ML14043A056

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IR 05000275-13-005, 05000323-13-005; on 09/22/2013 - 12/31/2013; Diablo Canyon Power Plant; Follow-up of Events and Notices of Enforcement Discretion
ML14043A056
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 02/11/2014
From: Walker W C
NRC/RGN-IV/DRP/RPB-A
To: Halpin E D
Pacific Gas & Electric Co
References
IR-13-005
Download: ML14043A056 (42)


See also: IR 05000275/2013005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION REGION IV 1600 E. LAMAR BLVD. ARLINGTON, TX 76011-4511

February 11, 2014

Mr. Edward D. Halpin

Senior Vice President and

Chief Nuclear Officer Pacific Gas and Electric Company

Diablo Canyon Power Plant

P.O. Box 56, Mail Code 104/6

Avila Beach, CA 93424

SUBJECT: DIABLO CANYON POWER PLANT

- NRC INTEGRATED

INSPECTION REPORT 05000275/2013005

and 05000323/2013005

Dear Mr. Halpin: On December 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Diablo Canyon Power Plant. On January 16 and February 7, 2014, the NRC inspectors discussed the results of this inspection with you and members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented three

findings of very low safety significance (Green) in this report. Two of these findings involved violations of NRC requirements. Further, inspectors documented

a licensee-identified violation which was determined to be of very low safety significance. The

NRC is treating this

violation as a non-cited violation

consistent with Section 2.3.2.a of the

Enforcement Policy. If you contest the violations or significance of these

NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region IV; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Diablo Canyon Power Plant.

If you disagree with the cross-cutting aspects assignment or the finding not associated with a

regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the Diablo Canyon Power Plant.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding," a copy of this letter, its enclosure, and your

response (if any) will be available electronically

for public inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's

E. Halpin - 2 - Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/ Wayne C. Walker, Branch Chief

Project Branch A

Division of Reactor Projects

Docket Nos.: 05000275, 05000323

License Nos.: DPR-80, DPR-82

Enclosure:

NRC Inspection Report 05000275/2013005 and 05000323/2013005 w/ Attachment: Supplemental Information

cc w/ Enclosure: Electronic Distribution

ML14043A056 SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials WCW Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials WCW

SRI:DRP/A RI:DRP/D RI:DRP/F SPE:DRP/A C:DRS/EB1 C:DRS/EB2 TRHipschman BDParks WCSmith RDAlexander TRFarnholtz GBMiller /RA/ via Email /RA/ via Email /RA/ via Email /RA/ /RA/ /RA/ 2/10/14 2/6/14 2/6/14 2/7/14 1/29/14 2/7/14 C:DRS/OB C:DRS/PSB1 C:DRS/PSB2 C:DRS/TSB

BC:DRP/A VGaddy MSHaire HGepford RKellar WWalker /RA/ /RA/ /RA/ /RA/ /RA/

2/10/14 2/10/14 2/10/14 2/10/14 2/11/14

- 1 - Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 05000275; 05000323 License: DPR-80; DPR-82

Report: 05000275/2013005;

05000323/2013005 Licensee: Pacific Gas and Electric Company Facility: Diablo Canyon Power Plant, Units 1 and 2 Location: 7 1/2 miles NW of Avila Beach Avila Beach, CA Dates: September 22 through December 31, 2013

Inspectors: T. Hipschman, Senior Resident Inspector G. Guerra, Emergency Preparedness Inspector, Plant Support Branch 1

R. Kumana, Resident Inspector, Projects Branch A J. Laughlin, Emergency Preparedness Inspector, NSIR B. Parks, Resident Inspector

C. Smith, Resident Inspector

Approved By: Wayne Walker Chief, Project Branch A

Division of Reactor Projects

- 2 - SUMMARY IR 05000275/2013005, 05000323/2013005; 09/22/2013 - 12/31/2013; Diablo Canyon Power Plant; Follow-up of Events and Notices of Enforcement Discretion

The inspection activities described in this report were performed between September 22, 2013,

and December 31, 2013, by the resident inspectors at Diablo Canyon Power Plant along with

two inspectors from the NRC's Region IV office and inspectors from other NRC offices. Three findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements.

The significance of in

spection findings is indicated by their color (Green, White, Yellow, or Red), which is determined using Inspection

Manual Chapter 0609, "Significance Determination Process." Their cross-cutting aspects are

determined using Inspection Manual Chapter 0310, "Components Within the Cross-Cutting Areas." Violations of NRC requirements are dispositioned in accordance with the NRC~s Enforcement Policy. The NRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process."

Cornerstone: Initiating Events

  • Green. The inspectors reviewed a Green self-revealing non-cited violation of 10 CFR 50.65(a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," for failure to implement adequate oversight controls and risk

assessment while performing 500kV transmission line insulator maintenance on Unit 2. This

caused an initiating event due to a flashover on the main transformer lightning arrester that resulted in a reactor trip. The failure to effectively perform a risk assessment and properly control maintenance activities that resulted in a reactor trip was a performance deficiency. The performance

deficiency was more than minor because it was associated with the human performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenged critical

safety functions during power operations, and is therefore a finding. Using Inspection

Manual Chapter 0609, Attachment 04, "Initial Characterization of Findings," and Appendix A,

Exhibit 1, "Initiating Events Screening Questions," this finding was determined to be of very low safety significance (Green) because, although it resulted in a reactor trip, it did not result in the loss of mitigating equipment relied upon to transition the plant from the onset of the

trip to a stable shutdown condition. Additionally, using Inspection Manual Chapter 0612,

Appendix K, "Maintenance Risk Assessment and Risk Management Significance

Determination Process," this finding was determined to be of very low safety significance (Green). The licensee entered the condition into the corrective action program as

Notification 50572800. This finding had a cross-cutting aspect in the area of human performance, associated with the decision-making component, because the licensee did not demonstrate that nuclear

safety was an overriding priority during this maintenance activity. Specifically, the licensee did not initially use conservative decision maki

ng in not properly categorizing the activity as a reactor trip risk (despite internal and external operating experience to the contrary), and

again when the licensee did not terminate the hot washing activities when environmental

conditions degraded resulting in excessive water dispersion H.1(b). (Section 4OA3.1)

- 3 - * Green. The inspectors reviewed a Green self-revealing finding due to an inadequate procedure for calibrating non-vital bus relays. This caused an initiating event due to a main feed pump trip and unplanned downpower transient to 50 percent power on Unit 1.

The licensee's failure to maintain an adequate maintenance procedure for calibrating non-vital bus relays is a performance deficiency. Specifically, the procedure was inadequate in

that it contained an optional step to position a cut-out switch so that the relay would not de-

energize the bus if actuated during maintenance activities. The performance deficiency was

more than minor because, if left uncorrected, the performance deficiency had the potential

to lead to a more significant safety concern. In particular, when the bus de-energized and tripped the running control oil pump, and the accumulator was unable to maintain system pressure while the back-up control oil pump reached operating pressure, the main feed

pump tripped which resulted in a reactor power transient greater than 20 percent. Using

Inspection Manual Chapter 0609, Attachment 04, "Initial Characterization of Findings," and

Appendix A, Exhibit 1, "Initiating Events Screening Questions," this finding was determined to be of very low safety significance (Green) because, although it resulted in a reactor transient, it did not result in the loss of mitigating equipment relied upon to transition the

plant from the onset of the trip to a stable shutdown condition. This finding was entered into

the corrective action program as Notification 50588799.

This finding had a cross-cutting aspect in the area of human performance, associated with the work control component, because the licensee did not adequately plan and coordinate

maintenance activities. Specifically, the licensee did not appropriately assess the job site conditions that could impact human performanc

e and human-system interface by failing to incorporate operating experience into procedural guidance H.3(a). (Section 4OA3.2)

Cornerstone: Barrier Integrity

  • Green. The inspectors reviewed a Green self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," after the licensee performed a design change to the control room ventilation system (CRVS) that resulted in none of the

four CRVS pressurization fans being able to continuously operate if they started in response

to a Phase A containment isolation or control room radiation atmosphere intake actuation signal. This resulted in declaring the Units 1 and 2 CRVS actuation instrumentation and CRVS inoperable and unplanned entry into Technical Specifications (TS) 3.3.7, "Control

Room Ventilation System Actuation Instru

mentation," and TS 3.7.10, "Control Room Ventilation System," respectively. The failure to use proper design control during the CRVS modification was a performance deficiency. The performance deficiency was more than minor because it was associated

with the human performance attribute of the Barrier Integrity cornerstone, and it adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radiological releases caused by accidents or events, and is

therefore a finding. Using Inspection Manual Chapter 0609, Attachment 04, "Initial

Characterization of Findings," and Appendix A, Exhibit 3, "Barrier Integrity Screening

Questions," this finding was determined to be of very low safety significance (Green)

because only the radiological barrier function of the control room was affected. The licensee

entered the condition into the corrective action program as Notification 50525605.

- 4 - The finding had a cross-cutting aspect in the area of human performance resources component because licensee staff did not maintain complete, accurate, and up-to-date design documentation - specifically, because the functions of the pressure switches and CRVS interlocks had never been adequately described in design control documents H.2(c).

(Section 4OA3.3)

Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into

the licensee's corrective action program. This violation and associated corrective action

tracking numbers are listed in Section 4OA7 of this report.

- 5 - PLANT STATUS

Unit 1 began the inspection period at essentially full power. On October 14, 2013, power was reduced to 50 percent due to an unplanned loss of a main feedwater pump. Following

corrective maintenance, the unit returned to full power on October 17, 2013. On October 28,

Unit 1 commenced a controlled power reduction to 50 percent for planned circulating water

tunnel cleaning. Unit 1 returned to full power on November 3, 2013, and remained there for the

duration of the inspection period.

Unit 2 essentially remained at full power the entire inspection period.

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01) .1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

On December 12 and December 20, 2013, the inspectors completed an inspection of the station's readiness for seasonal extreme weather conditions. The inspectors reviewed the licensee's adverse weather procedures for high winds and evaluated the licensee's implementation of these procedures. The inspectors verified that prior to high winds, the

licensee had corrected weather-related equipment deficiencies identified during the

previous winter.

The inspectors selected two risk-significant systems that were required to be protected

from high winds:

  • 500kV offsite power
  • Unit 2 start-up transformer

The inspectors reviewed the licensee's procedures and design information to ensure the

systems and components would remain functional when challenged by adverse weather. The inspectors verified that operator actions described in the licensee's procedures were

adequate to maintain readiness of these systems.

These activities constituted one sample of readiness for seasonal adverse weather, as

defined in Inspection Procedure 71111.01. b. Findings

No findings were identified.

- 6 - .2 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

On October 8, 2013, the inspectors completed an inspection of the station's readiness for impending adverse weather conditions. The inspectors reviewed plant design

features, the licensee's procedures and planned actions to respond to the season's first

rain, and the licensee's planned implementation of these procedures. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant.

These activities constituted one sample of readiness for impending adverse weather

conditions, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

.3 Readiness to Cope with External Flooding

a. Inspection Scope

On November 3, 2013, the inspectors completed an inspection of the station's readiness to cope with external flooding. After reviewing the licensee's flooding analysis, the

inspectors chose two plant areas that were susceptible to flooding:

  • Unit 1 auxiliary salt water rooms
  • Unit 2 auxiliary salt water rooms

The inspectors reviewed plant design features and licensee procedures for coping with

flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether credited operator actions could be successfully accomplished.

These activities constituted one sample of readiness to cope with external flooding, as

defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04) .1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant systems: * September 24, 2013, Unit 2, emergency diesel generator 2-2

- 7 - * November 3, 2013, Unit 1, auxiliary salt water system

The inspectors reviewed the licensee's procedures and system design information to

determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constituted two partial system walk-down samples as defined in

Inspection Procedure 71111.04.

b. Findings

No findings were identified.

.2 Complete Walkdown

a. Inspection Scope

On November 22, 2013, the inspectors performed a complete system walk-down inspection of the auxiliary feedwater pump 1-1. The inspectors reviewed the licensee's procedures and system design information to

determine the correct auxiliary feedwater lineup for the existing plant configuration. The inspectors also reviewed outstanding

work orders, open condition reports, in-process design changes, temporary

modifications, and other open items tracked by the licensee's operations and engineering departments. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.

These activities constituted one complete system walk-down sample, as defined in

Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05) .1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensee's fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas

important to safety:

  • October 1, 2013, Unit 1 and 2, fire areas 6-A-1, 6-A-2, 6-A-3, 6-B-1, 6-B-2, 6-B-3
  • October 29, 2013, Units 1 and 2 intake structure

For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensee's fire protection program. The inspectors

- 8 - evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constituted four quarterly inspection samples, as defined in Inspection

Procedure 71111.05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06) a. Inspection Scope

The inspectors completed an inspection of the station's ability to mitigate flooding due to internal causes. After reviewing the licensee's flooding analysis, the inspectors chose two plant areas containing risk-significant structures, systems, and components that

were susceptible to flooding:

  • November 4, 2013, Units 1 and 2, auxiliary salt water pump vaults
  • November 6, 2013, Unit 1, component cooling water heat exchanger room 1-1

The inspectors reviewed plant design features and licensee procedures for coping with

internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be

successfully accomplished.

These activities constitute completion of two flood protection measures samples as

defined in Inspection Procedure 71111.06.

b. Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07) a. Inspection Scope

On December 20, 2013, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors reviewed the data from a

performance test for the Unit 2 containment fan cooler units.

These activities constitute completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07. b. Findings

No findings were identified.

- 9 - 1R11 Licensed Operator Requalification Program and Licensed Operator Performance (71111.11)

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On October 18, 2013, the inspectors observed a crew of licensed operators in the plant's simulator during requalification testing. The inspectors assessed the following areas:

  • Licensed operator performance
  • The ability of the licensee to administer the evaluations
  • The quality of post-scenario critiques

These activities constitute completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

On October 14, 2013, and October 28, 2013, the inspectors observed the performance of on-shift licensed operators in the plant's main control room. At the time of the observations, the plant was in a period of heightened activity due to reductions in plant

power. The inspectors observed the operators' performance of the following activities:

  • Unit 1 post transient runback to 50 percent following the trip of main feed

pump 1-1 * Unit 1 curtailment to 50 percent power for circulating water tunnel and condenser cleaning

In addition, the inspectors assessed the operators' adherence to plant procedures,

including conduct of operations procedures and other operations department policies.

These activities constitute completion of two quarterly licensed operator performance

samples, as defined in Inspection Procedure 71111.11. b. Findings

No findings were identified.

- 10 - 1R12 Maintenance Effectiveness (71111.12) a. Inspection Scope

The inspectors reviewed one instance of degraded performance or condition of safety-related structures, systems, and components (SSCs):

  • December 23, 2013, Units 1 and 2, plant radiation monitors The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors

reviewed the licensee's work practices to evaluate whether these may have played a

role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule) and verified that the licensee was appropriately tracking degraded performance

and conditions in accordance with the Maintenance Rule.

These activities constituted completion of one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) a. Inspection Scope

On October 10, 2013, the inspectors revi

ewed a risk assessment performed by the licensee prior to a planned change in plant configuration and the risk management

actions planned by the licensee in response to elevated risk due to tracking on 230kV transformers and the need for insulator cleaning.

The inspectors verified that this risk assessment was performed timely and in

accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant

procedures. The inspectors reviewed the accuracy and completeness of the licensee's

risk assessment and verified that the licensee implemented appropriate risk management actions based on the result of the assessment.

On October 11, 2013, the inspectors observed portions of emergent work activities that

had the potential to affect the functional capability of mitigating systems due to a failed

stroke time test on auxiliary feedwater valve LCV-110.

The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to

minimize the impact of the work activities on unaffected structures, systems, and

components (SSCs).

These activities constitute completion of two maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

- 11 - b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15) a. Inspection Scope

The inspectors reviewed six operability determinations that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs):

transformer pump 0-2 The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operable, the

inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the

degraded SSC.

These activities constitute completion of six operability and functionality review samples,

as defined in Inspection Procedure 71111.15. b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18) a. Inspection Scope

On December 5, the inspectors reviewed a permanent plant modification to the Unit 2

plant computer system.

- 12 - The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or

other unplanned event. The inspectors verified that post-modification testing was

adequate to establish the functionality of the structures, systems, or components as

modified.

These activities constitute completion of one sample of permanent modifications, as defined in Inspection Procedure 71111.18. b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19) a. Inspection Scope

The inspectors reviewed four post-maintenance testing activities that affected risk-significant structures, sy

stems, or components (SSCs):

The inspectors reviewed licensing- and design-basis documents for the SSCs and the

maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constitute completion of four post-maintenance testing inspection

samples, as defined in Inspection Procedure 71111.19. b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22) a. Inspection Scope

The inspectors observed four risk-significant surveillance tests and reviewed test results

to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions:

- 13 - Inservice tests:

pump 1-2 Other surveillance tests:

  • October 17, 2013, Functional Test of Unit 1 anticipated transient without scram mitigation system actuation circuitry
  • December 23, 2013, Unit 1, surveillance test of emergency diesel generator 1-3 The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria.

These activities constitute completion of four surveillance testing inspection samples, as

defined in Inspection Procedure 71111.22. b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness 1EP2 Alert and Notification System Testing (71114.02) a. Inspection Scope

The inspectors discussed with licensee staff the operability of offsite siren emergency warning systems and backup alerting methods to determine the adequacy of licensee methods for testing the alert and notification system in accordance with 10 CFR Part 50,

Appendix E. The licensee's alert and notification system testing program was compared

with criteria in NUREG-0654, "Criteria for Preparation and Evaluation of Radiological

Emergency Response Plans and Preparedness in Support of Nuclear Power Plants," Revision 1; FEMA Report REP-10, "Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants," and the licensee's current FEMA-approved alert

and notification system design report, "Alert and Notification Design Report," Revision 1.

The specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71114.02.

b. Findings

No findings were identified.

- 14 - 1EP3 Emergency Response Organization Staffing and Augmentation System (71114.03) a. Inspection Scope

The inspectors discussed with licensee staff the operability of primary and back-up systems for augmenting the on-shift emergency response staff to determine the

adequacy of licensee methods for staffing emergency response facilities in accordance

with the requirements of 10 CFR Part 50, Appendix E. The inspectors reviewed licensee methods for staffing alternate emergency response facilities. The inspectors also reviewed periodic surveillances of the augmentation system to determine the licensee's

ability to staff emergency response facilities within the response times described in the

site emergency plan. The specific documents reviewed during this inspection are listed

in the attachment.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.03.

b. Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The Office of Nuclear Security and Incident Response (NSIR) headquarters

staff performed an in-office review of the latest revisions of various Emergency Plan

Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS

accession numbers ML13269A256 and ML13277A112 as listed in the Attachment.

The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to

10 CFR Part 50. The NRC review was not documented in a safety evaluation report and

did not constitute approval of licensee-generated changes; therefore, this revision is

subject to future inspection. The specific documents reviewed during this inspection are listed in the Attachment.

These activities constitute completion of three samples as defined in Inspection

Procedure 71114.04 05.

b. Findings

No findings were identified.

- 15 - 1EP5 Maintenance of Emergency Preparedness (71114.05)

a. Inspection Scope

The inspectors reviewed licensee records associated with maintaining the emergency

preparedness program between August 2011 and November 2013, including:

  • Licensee procedures
  • After-action reports
  • Quality Assurance audit and surveillance reports
  • Program assessments
  • Drill and exercise evaluation reports

The inspectors reviewed summaries of 725 corrective action program entries assigned

to the emergency preparedness department and emergency response organization and

selected 32 for detailed review against the program requirements. The inspectors

evaluated the response to the corrective action requests to determine the licensee's ability to identify, evaluate, and correct problems in accordance with the licensee program requirements, planning standard 10 CFR 50.47(b)(14), and 10 CFR Part 50,

Appendix E.

The inspectors reviewed summaries of 103 assessments of the impact of changes to the

emergency plan and emergency plan implementing procedures and selected 5 for detailed review against program requirements. The inspectors also visited the licensee's alternate emergency response facilities and reviewed their procedures for use when

access to the site is restricted. The specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71114.05.

b. Findings

Unresolved Item - Procedures for Recommending Protective Actions for Members of the Public on the Pacific Ocean

Introduction. The inspectors identified an unresolved item associated with the implementation of the licensee's process to make protective action recommendations

within the ten mile emergency planning zone (EPZ). This item remains unresolved

- 16 - pending further NRC staff review to determine if this issue constitutes a violation of NRC

requirements.

Description. The inspectors determined that the licensee does not make protective action recommendations for members of the public on the ocean within ten miles of the plant. The licensee also does not notify t

he United States Coast Guard (USCG) of emergency events. A requirement to make direct notifications was removed from the

licensee's emergency plan implementing procedures (EPIP) in 2003. The licensee relies

on the San Luis Obispo County government to notify the USCG to take any actions

necessary to protect members of the public. The county has procedures which include a default action to recommend the USCG evacuate waterborne vessels within five nautical miles if the licensee notifies the county

of a general emergency. The USCG has additional guidance recommending a two nautical mile "safety zone" for an alert or site

area emergency. The licensee had initiated a condition report on November 12, 2013, identifying that other sites make protective action recommendations for water areas. Title 10 of the Code of Federal Regulations Part 50.54(q)(2) requires the licensee to maintain an emergency plan that meets the planning standards outlined in

10 CFR 50.47(b). The planning standard outlined in 10 CFR 50.47(b)(10) requires the licensee to provide a range of protective actions for emergency workers and members of the public in the plume exposure pathway EPZ. NUREG-0654 generally defines the plume exposure EPZ as ten miles radius from the plant. The EPZ may

be defined with alternate boundaries by the licensee if an adequate basis exists.

Title 10 of the Code of Federal Regulations Part 50.54(q)(3) requires the licensee to obtain NRC approval for changes to the emergency plan, or perform an analysis demonstrating the changes do not reduce the effectiveness of the plan. The licensee

did not obtain prior NRC approval for the 2003 revision to the EPIPs removing the direct notification to the USCG of emergency declarations. This issue remains unresolved pending further NRC review of additional information to address the concerns described above, in order to determine the adequacy of the

licensee's emergency plan and implementing procedures, whether the licensee's protective actions recommendations procedure is consistent with their licensing basis, and whether or not the issue represents a violation of 10 CFR 50.54(q)(2). In addition,

more information is required to determine if the revision to the implementing procedures

removing the requirement to make a direct notification to the USCG constitutes a violation of 10 CFR 50.54(q)(3).

This issue is being tracked as URI 05000275/2013005-01; 05000323/2013005-01; "Unresolved Item - Procedures for Recommending Protective Actions for Members of the Public on the Pacific Ocean."

1EP6 Drill Evaluation (71114.06) Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on October 30, 2013, to verify the adequacy and capability of the licensee's assessment of drill performance. The

inspectors reviewed the drill scenario, observed the drill from the Technical Support

- 17 - Center, and reviewed the post-drill critique. The inspectors verified that the licensee's emergency classifications, off-site notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and

entered into the corrective action program for resolution.

These activities constitute completion of one emergency preparedness drill observation

sample, as defined in Inspection Procedure 71114.06-05.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security 4OA1 Performance Indicator Verification (71151) .1 Data Submission Issue

a. Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the third quarter 2013 performance indicators for any obvious inconsistencies prior to its

public release in accordance with Inspection Manual Chapter 0608, "Performance

Indicator Program."

This review was performed as part of the inspectors' normal plant status activities and, as such, did not constitute a separate inspection sample.

b. Findings

No findings were identified.

.2 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors reviewed the licensee's reactor coolant system chemistry sample analyses for the period of September 2012 through September 2013 to verify the

accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of

the reported data.

These activities constituted verification of the reactor coolant system specific activity performance indicator for Units 1 and 2, as defined in Inspection Procedure 71151.

- 18 - b. Findings

No findings were identified.

.3 Reactor Coolant System Identified Leakage (BI02)

a. Inspection Scope

The inspectors reviewed the licensee's records of reactor coolant system (RCS) identified leakage for the period of September 2012 through September 2013 to verify

the accuracy and completeness of the reported data. The inspectors reviewed the performance of RCS leakage surveillance procedure on October 7, 2013. The inspectors used definitions and guidance contained in Nuclear Energy Institute

Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7,

to determine the accuracy of the reported data.

These activities constituted verification of the reactor coolant system specific activity performance indicator for Units 1 and 2, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.4 Drill/Exercise Performance (EP01)

a. Inspection Scope

The inspectors sampled licensee submittals for the Drill and Exercise Performance, performance indicator for the period October 2012 through September 2013 to

determine the accuracy of the licensee's reported performance indicator data. The inspectors reviewed the licensee's records associated with the performance indicator to verify that the licensee accurately reported the indicator in accordance with relevant

procedures and Nuclear Energy Institute Document 99-02, "Regulatory Assessment

Performance Indicator Guideline," Revision 7. Specifically, the inspectors reviewed

licensee records and processes including procedural guidance on assessing opportunities for the performance indicator; assessments of performance indicator opportunities during pre-designated control room simulator training sessions,

performance during the 2012 biennial exercise, and performance during other drills. The

specific documents reviewed are described in the attachment to this report.

These activities constitute completion of the drill/exercise performance sample as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

- 19 - .5 Emergency Response Organization Drill Participation (EP02)

a. Inspection Scope

The inspectors sampled licensee submittals for the Emergency Response Organization Drill Participation performance indicator for the period October 2012 through

September 2013 to determine the accuracy of the licensee's reported performance

indicator data. The inspectors reviewed the licensee's records associated with the performance indicator to verify that the licensee accurately reported the indicator in accordance with relevant procedures and Nuclear Energy Institute Document 99-02,

"Regulatory Assessment Performance Indicator Guideline," Revision 7. Specifically, the

inspectors reviewed licensee records and processes including procedural guidance on

assessing opportunities for the performance indicator, rosters of personnel assigned to key emergency response organization positions, and exercise participation records. The specific documents reviewed are described in the attachment to this report.

These activities constitute completion of the emergency response organization drill

participation sample as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.6 Alert and Notification System Reliability (EP03)

a. Inspection Scope

The inspectors sampled licensee submittals for the Alert and Notification System performance indicator for the period October 2012 through September 2013 to

determine the accuracy of the licensee's reported performance indicator data. The

inspectors reviewed the licensee's records associated with the performance indicator to

verify that the licensee accurately reported the indicator in accordance with relevant procedures and Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7. Specifically, the inspectors reviewed

licensee records and processes including procedural guidance on assessing

opportunities for the performance indicator and the results of periodic alert notification

system operability tests. The specific documents reviewed are described in the

attachment to this report.

These activities constitute completion of the alert and notification system sample as

defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

- 20 - 4OA2 Problem Identification and Resolution (71152) .1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensee's corrective action program. The inspectors verified that

licensee personnel were identifying problems at an appropriate threshold and entering

these problems into the corrective action program for resolution. The inspectors verified

that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensee's problem identification and resolution activities during the performance of the other

inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Semiannual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensee's corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. In particular, the inspectors focused their review on notifications

and several root cause reports completed in the last year which involved human performance issues, including:

  • Three instances of loss of start-up power (May 2011)
  • Low temperature overpressure protection inoperable to technician error (June 2012)
  • Reactor trip due to a high voltage insulator flashover (October 2012)
  • Control room ventilation system fans inadequate design modification (November 2012)
  • Inadvertent de-energizing of 4kV bus "G" (February 2013)
  • Containment isolation valve S-2-200 mispositioned during a mode change (March 2013)
  • 500kV insulator hot washing results in a reactor trip (July 2013)
  • Unit 2 spent fuel handling error (July 2013)
  • Main feed pump trip and reactor power transient due to inadvertent relay actuation (October 2013)
  • Auxiliary salt water cross tie valve found closed (November 2013)
  • Radiation monitors RM11 and 12 inoperable as a result of a maintenance activity (December 2013)

- 21 - The inspectors reviewed documents and interviewed personnel to determine if the licensee completely and accurately identified problems in a timely manner commensurate with its significance, evaluated and dispositioned operability issues, considered the extent of conditions and causes, prioritized the problem commensurate

with its safety significance, identified appropriate corrective actions, and completed

corrective actions in a timely manner commensurate with the safety significance of the issue. These activities constitute completion of one semi-annual trend review inspection sample as defined in Inspection Procedure 71152. b. Findings

No findings were identified. However, the inspectors identified that while the licensee appropriately identified and entered these individual issues into the corrective action

program, the root and apparent causes and associated corrective actions were limited in station-wide application. Specifically, the inspectors identified a common theme in the licensee's cause evaluations which focused on maintenance leadership not consistently

reinforcing human performance standards and error reduction tools. The licensee

agreed with the inspectors' observations and entered the issue into the corrective action

program as Notification 50601631, requiring a root cause evaluation to assess and take corrective actions relative to the adverse human performance trend more broadly than was completed for the individual station events. .3 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors selected three issues for an in-depth follow-up:

  • On October 22, 2013, the inspectors reviewed corrective actions associated with a Green non-cited violation issued in the first quarter of 2010 for failure to follow the requirements of the Seismically Induced System Interaction Program (SISIP) with respect to the stowage and anchoring of potential seismic hazards. The

inspectors evaluated the licensee's current compliance with the program, to

include a walkdown of locations in the plant and a review of a sample of required

seismic hazard evaluations. The inspectors assessed the licensee's problem identification threshold, cause analyses, extent of condition reviews and compensatory actions for the violation. The inspectors verified that the licensee

appropriately prioritized the planned corrective actions and that these actions

were adequate to correct the condition.

  • On November 27, 2013, the inspectors reviewed the diesel fuel oil storage and supply system components, particularly for the fuel oil flow transmitter FIT-168. The inspectors identified that this flow transmitter was found out of tolerance on several occasions, and that there were no preventative maintenance activities scheduled between surveillance tests of the fuel oil transfer system. The

inspectors interviewed the system engineer and reviewed the Maintenance

Rule (a).1 plan for planned corrective actions. In addition, the inspectors

independently verified that the inaccurate fuel flow readings from the FIT-168 fuel

- 22 - flow transmitter could not affect the surveillance test results, because separate fuel oil level indicators are used to verify the fuel system is transferring the proper amount of fuel oil.

  • The inspectors conducted a cumulative review of operator workarounds during the period December 2-6, 2012, for Units 1 and 2, and assessed the effectiveness of the operator workaround program to verify that the licensee was:

(1) identifying operator workaround problems at an appropriate threshold;

(2) entering them into the corrective action program; and (3) identifying and

implementing appropriate corrective actions. The review included walkdowns of the control room panels, interviews with licensed operators and reviews of the control room discrepancies list, the lit annunciators list, the operator burden list,

and the operator workaround list.

The inspectors assessed the licensee's problem identification threshold, cause analyses, extent of condition reviews, and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions

were adequate.

These activities constitute completion of three annual follow-up samples, which included

one operator work-around sample.

b. Findings

No findings were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) 05000323/2013-005-01: Unit 2 Reactor Trip due to Lightning Arrester

Flashover

Introduction. The inspectors reviewed a Green self-revealing non-cited violation of 10 CFR 50.65(a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants" for failure to implement adequate oversight controls and risk assessment while performing 500kV transmission line insulator maintenance on Unit 2. This caused an initiating event due to a flashover on the main transformer lightning arrester that resulted in a reactor trip.

Description. On July 10, 2013, with Diablo Canyon Power Plant Unit 2 at 100 percent power, PG&E personnel were performing periodic hot washing of 500kV transmission

line insulators. The purpose of hot washing the insulators is to remove contaminants

that can degrade the mechanical and insulating properties which could result in a flashover. A flashover is a high voltage short-circuit to ground event. During the hot washing of the Unit 2 500kV Phase A dead-end insulators, an overspray of wash water

drifted onto the 500kV main transformer Phase A lightning arrester, resulting in a

flashover to ground. This actuated the 500kV differential protection relay, which opened

the Unit 2 main generator output breakers as designed. This resulted in a Unit 2 main

turbine trip, and a reactor protection reactor trip, also as designed. The reactor protection system and engineered safeguards features performed as expected, and operators placed Unit 2 in a hot shutdown condition. There were no complications other

- 23 - than damage to the A Phase lightning arrester. Following repairs, Unit 2 was returned to

service on July 14, 2013. The inspectors reviewed the licensee's root-cause evaluation, as well as conducted an independent review. The inspectors determined the licensee appropriately identified that the root cause of the flashover event was a result of inadequate controls that lead to wash water drifting on the A Phase lightning arrester. The water stream overspray

containing dissolved dirt and sea salts was driven by wind onto the lightning arrester,

overloading its ability to provide adequate resistance to ground, which resulted in a

flashover. PG&E personnel did not take appropriate controls to stop the hot washing activity during a period when wind conditions resulted in excessive water dispersion, fogging, or overspray, contrary to PG&E transmission line washing requirements and techniques. Additionally, the licensee failed to adequately assess the maintenance risk by categorizing the activity as a non-trip risk. Conflicting guidance and a change to

procedure AD7.DC6, "On-line Maintenance Risk Management," resulted in licensee staff

inappropriately categorizing the hot wash activity as a non-trip risk, when it should have

been classified as a low trip risk. The basis for the hot washing preventative maintenance was not properly documented in the licensee preventive maintenance procedure, MA1.DC51. Because of this, the risk assessment changed over time from

being characterized as a trip risk, to a non-trip risk. The trip risk was screened out per

Procedure AD7.DC6, "On-line Maintenance Risk Management," as an activity which could not directly cause a reactor trip. Guidance in Section 3.15 of Procedure AD7.DC6 defined a risk activity as something that can significantly increase the probability of a reactor or turbine trip. Additionally, PG&E Grid Control Center operations routinely listed

hot washing as a trip risk. Further, the licensee did not identify several industry and

internal PG&E Electric Operations operating experience events that identified the potential for a flashover due to hot washing activities. The inspectors reviewed the licensee's corrective actions which included suspending hot washing activities. Diablo Canyon personnel began hot washing the 500kV insulators at a six-week frequency in 1996 in response to a failed insulator at a PG&E substation. Prior to 1996, the 500kV dead-end insulators were washed during refueling outages.

As a result of this event, Diablo Canyon staff analyzed the periodicity of performing the

500kV insulators hot washes. The licensee determined that based on operating

experience and existing design, the insulators have sufficient margin to defer the maintenance activity until the next refueling outage.

Analysis. The failure to effectively perform a risk assessment and properly control maintenance activities that resulted in a reactor trip on July 10, 2013, was a performance deficiency. The performance deficiency was more than minor because it was associated

with the human performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant

stability and challenged critical safety functions during power operations, and is therefore

a finding. Using Inspection Manual Chapter 0609, Attachment 04, "Initial Characterization of Findings," and Appendix A, Exhibit 1, "Initiating Events Screening Questions," this finding was determined to be of very low safety significance (Green)

because, although it resulted in a reactor trip, it did not result in the loss of mitigating

equipment relied upon to transition the plant from the onset of the trip to a stable

- 24 - shutdown condition. Additionally, using Inspection Manual Chapter 0612, Appendix K, "Maintenance Risk Assessment and Risk Management Significance Determination

Process," this finding was determined to be of very low safety significance (Green). This finding had a cross-cutting aspect in the area of human performance, associated with the decision-making component, because the licensee did not demonstrate that nuclear safety was an overriding priority during this maintenance activity. Specifically, the

licensee did not initially use conservative decision making in not properly categorizing

the activity as a reactor trip risk (despite internal and external operating experience to

the contrary), and again when the licensee did not terminate the hot washing activities when environmental conditions degraded result

ing in excessive water dispersion.

H.1(b) Enforcement. This finding is also a violation of 10 CFR 50.65(a)(4), which requires that before performing maintenance activities including, but not limited to, surveillance,

post-maintenance testing, and corrective and preventive maintenance, the licensee shall

assess and manage the increase in risk that may result from the proposed maintenance

activities. The scope of the assessment includes non-safety-related structures, systems

and components whose failure could cause a reactor scram or actuation of a safety-related system. Contrary to this requirement, the licensee failed to assess the maintenance activity as a reactor trip initiating event by classifying the activity as a

non-trip risk. Because this finding was of very low safety significance and was entered

into the corrective action program as Notification 50579100, this violation is being

treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000323/20130055-02, "Reactor Trip due to a Lightning Arrester Flashover." .2 (Closed) LER 05000275/2013-007-00: Auxiliary Feedwater Actuation Due to a Main Feedwater Pump Trip

Introduction. The inspectors reviewed a Green self-revealing finding due to an inadequate procedure for calibrating non-vital bus relays. This caused an initiating event

due to a main feed pump trip and unplanned downpower transient to 50 percent power

on Unit 1.

Description. On October 14, 2013, with Unit 1 at 100 percent power, main feedwater pump 1-1 tripped. This event began when maintenance technicians inadvertently

contacted a 480V bus overcurrent relay. When the relay tripped, the non-vital 480V bus 15D de-energized. As a result, the inservice control oil pump tripped, and the backup control oil pump started as designed; however, a degraded control oil system

accumulator was not able to maintain control oil system pressure long enough for the

back-up control oil pump to develop pressure before the main feed pump 1-1 protective

logic tripped the pump. In response, plant operators rapidly reduced power from 100 percent to 50 percent power and manually started the auxiliary feedwater pumps per plant procedures and conditions. Feedwater and turbine control systems operated as designed, mitigating the loss of a single feed pump from full power. Diablo Canyon personnel determined that the cause of the relay trip was failure to incorporate operating experience in the relay maintenance procedure. Operating

experience documented that it was possible for the relay cover's reset arm to come into

contact with the relay during replacement of the cover following the calibration. The

- 25 - calibration procedure contained an optional step to position a cut-out switch so that the relay would not de-energize the bus if actuated. Although technicians discussed whether they should reposition the switch, they determined it was not necessary. The technicians were unaware that the cover lever could come in contact with the relay and

actuate the trip circuit. Inadequate procedural guidance and not incorporating operating experience were identified as causes for the unintended bus de-energization. Normally, a single bus de-energization should not result in a plant power transient because plant systems have backup or redundant equipment to provide for reliability. Although the main feed pump 1-1 back-up oil pump started as designed upon the loss of the running control oil pump, the control oil accumulator did not maintain system pressure as designed, resulting in the protective action to trip the main feed pump.

PG&E missed an opportunity to identify and correct the degraded accumulator prior to

this event. On June 29, 2013, while preparing to exit a forced outage, main feed

pump 1-1 was placed into service. Operators noticed an abnormal low nitrogen

pressure on the accumulator and initiated a notification to resolve the problem. In the evaluation, engineering personnel did not fully identify the problem with the accumulator not maintaining pressure and did not provide an adequate corrective action before

returning it to service. This created a hidden system vulnerability when the bus 15D

de-energization tripped the running control oil pump and the accumulator was unable to

maintain system pressure while the back-up control oil pump reached operating pressure. Following this event, maintenance personnel replaced the accumulator bladder. Analysis. The licensee's failure to maintain an adequate maintenance procedure for calibrating non-vital bus relays is a performance deficiency. Specifically, the procedure

was inadequate in that it contained an optional step to position a cut-out switch so that

the relay would not de-energize the bus if actuated during maintenance activities. The

performance deficiency was more than minor because, if left uncorrected, the performance deficiency had the potential to lead to a more significant safety concern. In particular, when the bus de-energized and tripped the running control oil pump, and the

accumulator was unable to maintain system pressure while the back-up control oil pump

reached operating pressure, the main feed pump tripped which resulted in a reactor

power transient greater than 20 percent. Using Inspection Manual Chapter 0609,

Attachment 04, "Initial Characterization of Findings," and Appendix A, Exhibit 1, "Initiating

Events Screening Questions," this finding was determined to be of very low safety significance (Green) because, although it resulted in a reactor transient, it did not result

in the loss of mitigating equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition. This finding had a cross-cutting aspect in the area of human performance, associated with the work control component, because the licensee did not adequately plan and

coordinate maintenance activities. Specifically, the licensee did not appropriately assess the job site conditions that could impact human performance and human-system interface by failing to incorporate operating experience into procedural guidance. H.3(a)

Enforcement. This finding does not involve enforcement action because no regulatory requirement was identified. This finding was placed in the licensee's corrective action

program as Notifications 50598753, 50588110, and 50588799. Because this finding

does not involve a violation and is of very low safety significance (Green), it is identified

- 26 - as a finding: FIN 05000275/2013005-03, "Auxiliary Feedwater Actuation Due to a Main Feedwater Pump Trip." .3 (Closed) LER 05000275; 05000323/2012-008-00: Loss of Control Room Ventilation System Due to Inadequate Design Control

Introduction. The inspectors reviewed a Green self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," after the licensee performed a design change to the control room ventilation system (CRVS) that resulted in none of the four CRVS pressurization fans being able to continuously operate if they started in

response to a Phase A containment isolation or control room radiation atmosphere

intake actuation signal. This resulted in declaring the Units 1 and 2 CRVS actuation

instrumentation and CRVS inoperable, and an unplanned entry into Technical Specification (TS) 3.3.7, "Control Room Ventilation System Actuation Instrumentation," and TS 3.7.10, "Control Room Ventilation System," respectively.

Description. In October 2012, Diablo Canyon personnel completed modifications and testing of the Units 1 and 2 CRVS by adding a back-draft damper in each unit's CRVS

recirculation line. These dampers were designed to minimize the amount of unfiltered air entering the control room when one train is not in operation. On November 27, 2012, while performing a functional test of the CRVS pressurization system, operators identified that none of the four CRVS pressurization fans would

continuously operate if they started in response to a safety injection or control room atmosphere intake radiation actuation signal. Operators declared the Units 1 and 2 CRVS actuation instrumentation inoperable and entered TS 3.3.7, "Control Room

Ventilation System Actuation Instrumentation," as directed by TS 3.3.7, Condition B,

operators also declared one train of CRVS inoperable and entered TS 3.7.10, Condition A. Licensee troubleshooting efforts determined that the recent installation of back-draft dampers and post-modification CRVS flow balancing resulted in a higher static head in CRVS common ducting during recirculation operation. This caused pressurization fan cycling due to actuation of the system pressure switches. The original pressurization

system design utilized pressure switches to provide interlocks which precluded running

two fans simultaneously by causing the non-associated fan to shut off. This feature was

originally designed to protect against over pressurization of the system ducting. Soon after initial system construction, the pressurization fans were modified such that over-pressurization was no longer possible, but the pressure interlocks remained in the actuation circuitry. Per design basis document Design Criteria Memorandum

(DCM) S-23F, "Control Room HVAC System," the pressure switches were only identified as providing a low pressure permissive to start a redundant fan. Therefore, engineers

involved in the damper modification and flow rebalancing did not recognize that the same pressure switches also provided an over-pressurization interlock. Following these modifications, the pressurization fan that was selected to run increased static pressure in

ducting downstream of the pressurization fans enough to exceed the setpoint of all the

pressure switches that indicate their associated fan is running. Thus, this condition

caused the operating fan to shut down, which lowered the common-header static

pressure below the setpoint of the pressure switch. This reduction of static pressure in the common header resulted in the restart of the pressurization fan. Thus, with the on-

- 27 - and-off cycling of the pressurization fan, the control room ventilation recirculation mode would not be sustained upon a Phase A containment isolation or radiation monitor actuation. However, Mode 4 CRVS operation could be sustained by control room operator manual action taken as directed by DCPP Emergency Operating

Procedure E-0, "Reactor Trip or Safety Injection," Appendix E, "ESP Auto Actions, Secondary and Auxiliaries Status." Analysis. The failure to use proper design control during the CRVS modification was a performance deficiency. The performance deficiency was more than minor because it

was associated with the human performance attribute of the Barrier Integrity cornerstone, and it adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radiological releases

caused by accidents or events, and is therefore a finding. Using Inspection Manual

Chapter 0609, Attachment 04, "Initial Characterization of Findings," and Appendix A,

Exhibit 3, "Barrier Integrity Screening Questions," this finding was determined to be of

very low safety significance (Green) because only the radiological barrier function of the control room was affected. The finding had a cross-cutting aspect in the area of human performance resources component because licensee staff did not maintain complete,

accurate, and up-to-date design documentation. Specifically, because the functions of

the pressure switches and CRVS interlocks had never been adequately described in design control documents. H.2(c)

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion III, "Design Control," requires, in part, that measures shall be established to assure that applicable regulatory requirements and the design basis, as defined in § 50.2 and as specified in the license application, for those structures, systems, and

components to which this appendix applies are correctly translated into specifications,

drawings, procedures, and instructions. Measures shall also be established for the

selection and review for suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of the structures, systems and components. Contrary to the above, in October 2012, the licensee completed a

design change to the control room ventilation system that resulted in none of the four

CRVS pressurization fans being able to continuously operate if they started in response

to a Phase A containment isolation or control room radiation atmosphere intake actuation

signal. This resulted in declaring the Units 1 and 2 CRVS actuation instrumentation and CRVS inoperable and an unplanned entry into Technical Specifications (TS) 3.3.7, "Control Room Ventilation System Actuation Instrumentation," and TS 3.7.10, "Control Room Ventilation System," respectively. Because this finding was of very low safety

significance and was entered into the corrective action program as Notification

50525605, this violation is being treated as a non-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 05000275;05000323/2012008-04, "Loss of Control Room Ventilation System Due to Inadequate Design Control."

.4 (Closed) Licensee Event Report (LER) 05000275/1-2013-004-00: All Three Unit 1 Emergency Diesel Generators Momentarily Inoperable On June 23, 2103, following a loss of 230kV offsite power, Unit 1 control room operators did not enter LCO 3.0.3 when they simultaneously made all three emergency diesel

generators inoperable by simultaneously placing them all in manual. When 230kV startup power to the site was lost due to an electrical fault on the grid, all diesel

- 28 - generators started automatically, as designed. The response procedure directs the operators to shut down the unloaded EDGs and place them in standby. The operators chose to first place all three EDG's in "manual," which makes them inoperable, and then shut them down and restored to "auto" one by one. This resulted in all three EDGs

being inoperable for approximately two minutes. The licensee identified this condition

the following day during a routine supervisory review, and subsequently followed up with

the required 8-hour non-emergency report to the NRC for an unanalyzed condition.

The inspectors dispositioned the failure to comply with technical specifications as a licensee identified violation in Section 4OA7 of this report.

No additional deficiencies were identified during the review of these Licensee Event

Reports supplemental revisions. This Licensee Event Report is closed.

These activities constitute completion of four event follow-up samples, as defined in Inspection Procedure 71153.

4OA6 Meetings, Including Exit Exit Meeting Summary

On November 21, 2013, the inspectors presented the results of the onsite inspection of the licensee's emergency preparedness program to Mr. T. Baldwin, Manager, Regulatory Services,

and other members of the licensee's staff. The licensee acknowledged the issues presented.

The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

On January 16, 2014, the inspectors presented the inspection results to Mr. E. Halpin, Senior

Vice President and Chief Nuclear Officer, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

On February 7, 2014, the inspectors presented additional information regarding the inspection

results to Mr. E. Halpin, Senior Vice President and Chief Nuclear Officer, and other members of

the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violations The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for being dispositioned as a non-cited violation.

shutdown initiated within one hour." Contrary to this, on June 23, 2013, following a loss

of 230kV offsite power, Unit 1 control room operators did not enter LCO 3.0.3 when they

simultaneously made all three EDGs inoperable by placing them all in manual. When

- 29 - 230kV startup power to the site was lost due to an electrical fault on the grid, all diesel generators started automatically, as designed. The response procedure directs the operators to shut down the unloaded EDGs and place them in standby. The operators chose to first place all three EDG's in "manual", which makes them inoperable, and then

shut them down and restored to "auto" one by one. This resulted in all three EDGs

being inoperable for approximately two minutes. The licensee identified this condition

the following day during a routine supervisory review and subsequently followed up with

the required 8-hour non-emergency report to the NRC for an unanalyzed condition. The performance deficiency was more than minor because it was associated with operating equipment lineup area of the configuration control attribute of the mitigating systems

cornerstone and affected the cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage). In accordance with IMC 0609 Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," this violation did not require a detailed risk evaluation because it did not represent an actual loss of diesel generator function for

greater than the Technical Specification allowed outage time, and the risk-significant

function was not lost, even though the design basis start would not have occurred.

Therefore, this violation was of very low safety significance (Green). The licensee entered the issue into the corrective action program as Notification 50570582. Corrective actions included implementing more stringent requirements for supervisory

oversight of plant manipulations and modifying the response procedure to specify sequential steps for placing EDGs in manual one at a time when securing.

A-1 Attachment SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

B. Allen, Site Vice President

J. Arhar, Supervisor, Engineering S. Baker, Manager, Engineering T. Baldwin, Manager, Regulatory Services

A. Bates, Director, Engineering Services

K. Bych, Manager, Engineering

S. Dunlap, Supervisor, Engineering J. Fledderman, Director, Strategic Projects P. Gerfen, Senior Manager

P. Gerfas, Assistant Director, Station Director

M. Gibbons, Acting Director, Work Control

M. Ginn, Manager, Emergency Planning D. Gouveia, Manager, Operations E. Halpin, Chief Nuclear Officer

D. Hardesty, Senior Engineer

J. Hinds, Director, Quality Verification

T. Irving, Manager, Radiation Protection

J. Kang, Engineer, Mechanical Systems Engineering T. King, Director, Nuclear Work Management

A. Lin, Engineering

J. MacIntyre, Director, Maintenance Services

M. McCoy, NRC Interface, Regulatory Services

J. Nimick, Director, Operations Services G. Porter, Senior Engineer J. Salazar, System Engineer

L. Sewell, Supervisor, Radiation Protection

D. Shippey, ALARA Supervisor, Radiation Protection

R. Simmons, Manager, Electrical Maintenance

D. Stermer, Manager, Operation M. Stevens, Associate, Quality Verification S. Stoffel, Supervisor, Dosimetry

J. Summy, Senior Director, Engineering and Projects

L. Walter, Station Support

J. Welsch, Station Director R. West, Manager, ICE Systems E. Wessel, Chemical Engineer, Chemistry M. Wright, Manager, Mechanical Systems Engineering

A-2 LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened 05000275/2013005-01

05000323/2013005-01 URI Procedures for Recommending Protective Actions for Members of the Public on the Pacific Ocean (Section 1EP5)

Opened and Closed

05000323/2013005-02

NCV Reactor Trip due to a Lightning Arrester Flashover (Section 4OA3.1)05000275/2013005-03

FIN Auxiliary Feedwater Actuation Due to a Main Feedwater Pump Trip (Section 4OA3.2)05000275/2012008-04

05000323/2012008-04 NCV Loss of Control Room Ventilation System due to Inadequate Design Control (Section 4OA3.3)

Closed 05000323/2-2013-005-

01 LER Unit 2 Reactor Trip due to Lightning Arrester Flashover (Section 4OA3.1)

05000275/1-2013-007-

00 LER Auxiliary Feedwater Actuation Due to a Main Feedwater Pump Trip (Section 4OA3.2) 05000275; 05000323/

1-2012-008-00 LER Loss of Control Room Ventilation System due to Inadequate Design Control (Section 4OA3.3)

05000275/1-2013-004-

00 LER All Three Unit 1 Emergency Diesel Generators Momentarily Inoperable (Section 4OA3.4)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

Number Title Revision OP J-2 Off-site Power Sources 9

Drawings Number Title Revision 502110 500/230/25/12/4kV Systems 19

A-3 Section 1R04: Equipment Alignment

Procedures

Number Title Revision OP J-6B:II-A Diesel Generator 2-2 Alignment Checklist 0 OP J-6B:II-A Diesel Generator 2-2 Alignment Checklist 0 OM6.ID13 Safety at Heights: Fall Protection, Ladder Safety, Working

Under Suspended Loads

18 OP D-1:II Auxiliary Feedwater System - Alignment Checklist 0

Drawings Number Title 102014 Piping Schematic-Somponent Cooling Water System

Section 1R05: Fire Protection

Procedures

Number Title Revision STP M-70C Inspection of ECG Doors 24 STP M-39A1 U1 & 2, Routine Surveillance Test of Diesel Generator 1-1 (2-1) Room Carbon Dioxide Fire System Operation

16 DCM S-18 Fire Protection System 13B OM8.ID4 Control of Flammable and Combustible Materials 20

OM8.ID1 Fire Loss Prevention 24 ECG 18.7 Fire Rated Assemblies 10

Drawings Number Title Revision 111906 Units 1 and 2 Fire Drawings, Sheets 1-32 6

Section 1R06: Flood Protection Measures

Work Orders

64079046 64065780

A-4 Section 1R07: Heat Sink Performance

Procedures

Number Title Revision STP M-51 Routine Surveillance Test of Containment Fan Cooler

Units January 20, 2013 STP M-51 Routine Surveillance Test of Containment Fan Cooler

Units March 10, 2013 STP M-93A Refueling Interval Surveillance - Containment Fan

Cooler March 13, 2013

Notifications

50592355

Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance

Procedures

Number Title Revision OP.1DC10 Conduct of Operations 39

Lesson R133S1 Fire in 480V Bus with Loss of Component Cooling Water Flow to Reactor Coolant Pumps

1a CP M-6 Fire 34 OP AP-11 Malfunction of Component Cooling Water System 30

EOP E-0 Reactor Trip or Safety Injection 43

Section 1R12: Maintenance Effectiveness

Miscellaneous

Title Revision Radiation Monitoring System Reliability and Availability October 29, 2013

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

Number Title Revision MA1.DC11 230kV Bare Hand Removal and Installation Drops October 10, 2013

A-5 Notifications

50578562

Section 1R15: Operability Determinations and Functionality Assessments

Procedures

Number Title Revision OM7.ID12 Operability Determination 27

OM7.ID13 Technical Evaluations 3 EOP E-2 Faulted Steam Generator Isolation 21 STP V-3P6A Exercising Valves LCV-110 and LCV-111 Auxiliary

Feedwater Pump Discharge

24 STP P-AFW-12 Routine Surveillance Test of Motor-Driven Auxiliary Feedwater Pump

18 STP I-92A AMSAC Functional Test 7 STP I-92A AMSAC Functional Test 8

STP M-21-A1

Emergency Diesel Generator Functional Test

95 STP M-9B Diesel Engine Generator Routine Surveillance Test 94

Notifications

50314416 50587512 50507137 50587869 50314416 A0662030 A0692213 A0735701 A0671415 A0479517 50577766 50577917 50572400 50573100 50572174

50595324 50591862 50594028 50594186 50595251

50596161 50596125 50590178 5058999

Section 1R19: Post-Maintenance Testing

Procedures

Number Title Revision STP M-9A Diesel Engine Generator Routine Surveillance Test 94 STP M-9B Diesel Engine Generator Routine Surveillance Test 94

STP P-AFW-22 Routine Surveillance Test of Motor-Driven Auxiliary Feedwater Pump 2-2

17

A-6 Work Orders

64103356 60052907 60053052 60053529 64045245 64085882 60056781 64050757 64052107 64080841 64089790 64089802 64091605 64103362 64057674

50439378

Section 1R22: Surveillance Testing

Procedures

Number Title Revision STP V-3P6A Exercising Valves LCV-110 and LCV-111 Auxiliary

Feedwater Pump Discharge

24 STP P-AFW-12 Routine Surveillance Test of Motor-Driven Auxiliary Feedwater Pump

18 STP I-92A AMSAC Functional Test 7 STP I-92A AMSAC Functional Test 8

Notifications

50587512 50507137 50587869 50314416

Section 1EP2: Alert and Notification System Testing

Procedures

Number Title Revision EP MT-43 Early Warning System And Maintenance 11

Miscellaneous

Number Title Revision Alert and Notification Design Report 0 Alert and Notification Design Report 1

P000129 Testing the MK 831DT Battery with the SOC 140 Battery Tester

A

A-7 Section 1EP3: Emergency Response Organization Staffing and Augmentation System

Procedure Number Title Revision EP EF-1 Activation And Operation Of The Technical Support

Center 44 EP EF-2 Activation And Operation Of The Operational Support

Center 33 EP EF-3 Activation And Operation Of The Emergency Operations Facility

37 Section 1EP4: Emergency Action Level and Emergency Plan Changes

Procedure Number Title Revision EP, Appendix F ERO On-Shift Staffing Analysis Report 4.00A

EP, Appendix D, Category S System Malfunction 4.01A EP, Section 7 Emergency Facilities and Equipment 4.18

Section 1EP5: Maintenance of Emergency Preparedness

Procedure Number Title Revision

AWP EP-007 Updating Letters of Agreement 0 EP EF-11 Operation of Alternate Emergency Response Facilities

0 EP EF-9 Backup Emergency Response Facilities 11 EP G-1 Emergency Classification and Emergency Plan

Activation

43 EP G-3 Notification of Off-Site Organizations 0 EP G-3 Notification of Offsite Organizations 2

EP G-3 Notification of Off-Site Agencies and Emergency Response Organization Personnel

39 EP G-3 Notification of Off-Site Agencies 40 EP G-3 Emergency Notification of Off-Site Agencies 54B EP G-4 Assembly and Accountability 26

A-8 Procedure Number Title Revision

EP G-5 Evacuation of Non-Essential Site Personnel 14 EP MT-27 Technical Support Center and Alternate Facility Location 13 EP MT-28 Operational Support Center and Alternate Facility Location 11 EP MT-29 Emergency Operations Facility (EOF) 10 EP RB-10 Protective Action Recommendations 10 EP RB-10 Protective Action Recommendations 16

EP RB-3 Stable Iodine Thyroid Blocking 7

OM10 Emergency Preparedness 2

OM10.DC1 Emergency Preparedness Drills and Exercises 6 OM10.DC2 Emergency Response Organization On-Call 6 OM10.DC3 Emergency Response Facilities, Equipment, and

Resources

6 OM10.ID2 Emergency Plan Revision and Review 11 OM10.ID4 Emergency Response Organization Management 12

OM7.ID1 Problem Identification and Resolution 43 OP1.DC17 Control of Equip Required by Technical Specifications or Designated Programs

27 OP1.DC37 Plant Logs 49 XI1.ID2 Regulatory Reporting Requirements and Reporting

Process 38 Miscellaneous

Number Title Revision Cal OES - Emergency Planning Zones for Serious Nuclear Power Plant Accidents

Emergency Plan 4 PSS25 USCG - DCPP Emergency Response November 2007

SOP III.01 San Luis Obispo County - Emergency Services

Director October 2012 SOP III.25 San Luis Obispo County - United States Coast Guard June 2013

A-9 Number Title Revision SOP III.44 San Luis Obispo County - Port San Luis Harbor District September 2012 DCL-03-024 Emergency Plan Implementing Procedure Update March 5, 2003 FN120390032 Emergency Preparedness Program Audit May 3, 2012

FN123390018 Emergency Preparedness Program Audit February 13, 2013

SAPN50527030 2013 DCPP Baseline Inspection Readiness Assessment Report

October 18, 2013

Condition Reports

50390230 50392157 50420772 50422636 50422848

50426267 50426528 50427067 50429569 50439297

50439409 50441513 50454155 50457490 50459012

50463112 50468358 50480569 50507869 50508628

50510467 50511677 50522732 50523461 50531921

50531922 50532391 50536699 50542191 50557886

50560263 50562023 50569770 50572410 50573151

50583556 50584094 50593750 50595533

Section 4OA1: Performance Indicator Verification

Procedure Number Title Revision AWP EP-001 Emergency Preparedness Performance Indicators 16 XI1.DC1 Collection and Submittal of NRC Performance

Indicators

12 STP R-10C Reactor Coolant System Water Inventory Balance 44

A-10 Section 4OA2: Problem Identification and Resolution

Procedures

Number Title Revision AD4.ID3 SISIP Housekeeping Activities 12 Seismically Induced Systems Interaction Manual 10 AD7.ID2 Daily Notification Review Team and Standard Plant Priority Assignment Scheme

20 AD7.ID12 Work Management Process 3

Notifications

50494799 50463051 50299740 50499634 50572174 50587627 50572355 50577917 50572400 50573100 50588799 50587467 50592711 50595324 50600007

50591862 50592561 50560387 50592561 50560826

50583459 50583562

Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion

Notifications

50572400 50573100 50572800

Section 4OA7: Licensee-Identified Violations

Notifications

50570582