LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl |
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Dear Sir:
Attached is Revision 1 to Licensee Event Report No. 81-20, concerning failure l
of the "B" Train Control Room Chlorine Detector unit. The corrective action originally taken to prevent binding of the motor shaft was apparently insuffi-cient as the same failure occurred again two months later. On this occasion, the corrective action taken was to replace the entire blower motor. The "A" Train Chlorine Detaction System was operable at all times, therefore, there was no effect on plant or public health and safety, a
Sincerely, l
C. P. Yundt General Manager CPY/MLD/KLN:mae Attachments c:
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UPDATE REPORT - DATE OF PREVIOUS REPORT October 6, 1981
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REPORTABLE OCCURRENCE 1.
Report No.:
81-20, Revision 1 g
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a.
Report Date:
December 11, 1981 b.
Occurrence Date: September 6 and November 11, 1981 4
3.
Facility: Trojan Nuclear Plant, P.O. Box 439 Rainier, OR 97048 4.
Identification of Occurrence:
During a routine plant tour, an Auxiliary Operator noticed that the blower to the Control Room "B" Chlorine Detector was not operating properly. Two months later, the same blower was discovered to have failed again.
l I
5.
Conditicns Prior to Occurrence:
i The plant was in Mode 1 at 1007. power and steady state operation on both occasions.
I 6.
Description of Occurrence:
l The Chloralert Blower Ibtor on the Chlorine Detector was not working properly, which rendered the detector inaperable. The unit is a Fischer-Porter Model 17CA1010 Chloralert Blower Motor.
7.
Designation of Apparent Cause of Occurrence:
The electric motor on the blower appeared to be binding as lubricant 4
applied to the motor bearing would free the blower for a short time.
l 8.
Analysis of Occurrence:
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I Inspection showed that a dirty bearing on the blower motor was causing l
the motor to bind. There was no ef fect on plant or public safety sines the "A" Train Control Room Chlorine Detector was operable.
9.
Corrective Action
Upon discovery, the detector was immediately taken out of service and the Contrcl Room ventilation was transferred to the emergency recirculation mode pcr S.T.S. 3.3.3.6.
The motor bearing was cleaned and lubricated, the flow metering tube was cleaned, and the detector was calibrated and returned to service on September 8,1981.
Following the seconi identical failure of the blower, the entire blower motor was replaced to prevent recurrence. Periodic inspection and cleaning of the chlorine Detector units has been added to the prevantive maintenance program.
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LICENSEE EVENT REPORT EXHIBIT A CcNTRot. steCm i f ! ! ! I fQ tetEAsE PRWT OR TYPE ALL REQUIRED WFORMATICM i
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e EVENT ossCRIPTION AND PRC8ASLE CCNSEQUENCES h'id gl AT FULL POWER OPERATION, AN OPERATOR DISCOVERED "B" TRAIN CONTROL ROOM i
[TTTl CHLORINE DETECTOR WAS NOT OPERATING' DURING A ROUTINE SHIFT TOUR.
THIS I
io!.ii FAILURE OCCURRED AGAIN ON NOVEMBER 11, 1981. TWO INDEPENDENT SYSTDfS ARE I f
f io isi t REQUIRED PER S.T.S. 3.3.3.6.
THE "A" TRAIN DETECTOR WAS OPERABLE. PROB- ;
i o,,, i l ABLE CONSEQUENCES WERE MINIMAL. THERE WAS NO EFFECT ON PUBLIC HEALTH OR g
lc#7i l SAFETY.
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.s s2 s2 CAUSE CESCRIPTION AND CQRRECf1VE ACTTCNS 27 l,
l, j a i l THE BEARING ON THE BLOWER MOTOR CAUSED IT TO BIND. THE DETECTOR WAS TAKEN,
I TT1 i OUT OF SERVICE AND CONTROL ROOM VENTILATION SWITCHED TO EMERGENCY RE-i
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[ CIRCULATION MODE. THE BEARING WAS LUBRICATED, METERING TUBE CLEANED, gl.AND DETECTOR CALIBRATED AND RETURNED TO SERVICE. FOLLOWING THE SECOND l
i,,.i t FAILURE, THE ENTIRE BLOWER MOTOR WAS REPLACED. PERIODIC CLEANING HAS 8,;ciuvv BEEN ADDED IO THE PREVEN VEgl g.pANCE PROGRAM.
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| 05000344/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000344/LER-1981-001-03, /03L-0:on 801212,blown Fuse Was Found in Breaker Control Power Circuit for Vent Supply Fan to turbine-driven Auxiliary Feedwater Pump Room.Cause Unknown.Fuse Replaced | /03L-0:on 801212,blown Fuse Was Found in Breaker Control Power Circuit for Vent Supply Fan to turbine-driven Auxiliary Feedwater Pump Room.Cause Unknown.Fuse Replaced | | | 05000344/LER-1981-002-03, /03L-0:on 810107,after Normal Sampling of RCS, Common Sample Containment Isolation Valve Failed to Close from Control Room.Caused by Inadequate Lubrication of Valve Stem.Valve Stem Cleaned & Lubricated | /03L-0:on 810107,after Normal Sampling of RCS, Common Sample Containment Isolation Valve Failed to Close from Control Room.Caused by Inadequate Lubrication of Valve Stem.Valve Stem Cleaned & Lubricated | | | 05000344/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000344/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000344/LER-1981-003-03, /03L-0:on 810130,min Required Number of Source Range Channels Not Met When Both Channels of Nuclear Source Range Indications Failed to Energize Automatically.Caused by Improper Actuation of Instrument Crowbar Circuit | /03L-0:on 810130,min Required Number of Source Range Channels Not Met When Both Channels of Nuclear Source Range Indications Failed to Energize Automatically.Caused by Improper Actuation of Instrument Crowbar Circuit | | | 05000344/LER-1981-004-03, /03L-0:on 810122,fan Cooling Unit for Pump Did Not Automatically Start During Periodic Operating Test of Containment Spray Pump B.Caused by Thermal Overload Trip on Fan Unit Supply Breaker B-2415.Overloads Reset | /03L-0:on 810122,fan Cooling Unit for Pump Did Not Automatically Start During Periodic Operating Test of Containment Spray Pump B.Caused by Thermal Overload Trip on Fan Unit Supply Breaker B-2415.Overloads Reset | | | 05000344/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000344/LER-1981-005-03, /03L-0:on 810305,valves MO-2052A & MO-2069A Forming Containment Boundary Between Containment Spray Sys & Recirculation Sump in Auxiliary Bldg Found Incorrectly Positioned.Caused by Personnel Error | /03L-0:on 810305,valves MO-2052A & MO-2069A Forming Containment Boundary Between Containment Spray Sys & Recirculation Sump in Auxiliary Bldg Found Incorrectly Positioned.Caused by Personnel Error | | | 05000344/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-006-03, /03L-0:on 810316,erratic Trip Setpoint Found on Engineered Safeguards Feature Steamline Pressure Channel 516.Caused by Failed Capacitator.Capacitator Replaced & Channel Calibr | 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Function.Damaged Breaker Repaired & Returned to Svc | /03L-0:on 810420,motor Control Ctr Power Lost When Worker Shorted Bus to Ground Causing Feed Breaker to Open.Caused by Personnel Error.Meter Set to Wrong Function.Damaged Breaker Repaired & Returned to Svc | | | 05000344/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-010, Forwards LER 81-010/03L.Detailed Event Analysis Encl | Forwards LER 81-010/03L.Detailed Event Analysis Encl | | | 05000344/LER-1981-010-03, /03L-0:on 810502,outer Door of Airlock at 93 Ft Elevation of Containment Was Left Open.Caused by Personnel Error.Personnel Retrained | /03L-0:on 810502,outer Door of Airlock at 93 Ft Elevation of Containment Was Left Open.Caused by Personnel Error.Personnel Retrained | | | 05000344/LER-1981-011-03, /03L-0:on 810629,local Leak Rate Testing Results Showed That Cumulative Leakage Through Type C Containment Valves Exceeded Sts.Causes & Corrective Actions Stated in Table 1.Valves Repaired & Retested Prior to Plant Heatup | /03L-0:on 810629,local Leak Rate Testing Results Showed That Cumulative Leakage Through Type C Containment Valves Exceeded Sts.Causes & Corrective Actions Stated in Table 1.Valves Repaired & Retested Prior to Plant Heatup | | | 05000344/LER-1981-011, Forwards LER 81-011/03L-0.Detailed Event Analysis Encl | Forwards LER 81-011/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-012-03, /03L-0:on 810626,during RCS Level Reduction, Operating RHR Pump Began Cavitating & Was Stopped to Prevent Pump Damage.Caused by Inadequate Venting of Pressurizer. Procedures Will Be Reviewed W/Personnel | /03L-0:on 810626,during RCS Level Reduction, Operating RHR Pump Began Cavitating & Was Stopped to Prevent Pump Damage.Caused by Inadequate Venting of Pressurizer. Procedures Will Be Reviewed W/Personnel | | | 05000344/LER-1981-012, Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | Forwards LER 81-012/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-013-03, /03L-0:on 810703,during RCS Integrity Test,Rcs Leakage Exceeded Tech Spec Limit.Caused by Leaking Drain Valves on Reactor Coolant Loops Due to Failure to Torque Valves | /03L-0:on 810703,during RCS Integrity Test,Rcs Leakage Exceeded Tech Spec Limit.Caused by Leaking Drain Valves on Reactor Coolant Loops Due to Failure to Torque Valves | | | 05000344/LER-1981-013, Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | Forwards LER 81-013/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-014-03, /03L-0:on 810728,during Routine Operator Surveillance at 80% Power,Main Containment Isolation Valve for Demineralized Water Washdown Found in Open Position. Caused by Personnel Negligence.Valve Closed & Locked | /03L-0:on 810728,during Routine Operator Surveillance at 80% Power,Main Containment Isolation Valve for Demineralized Water Washdown Found in Open Position. Caused by Personnel Negligence.Valve Closed & Locked | | | 05000344/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Event Analysis Encl | Forwards LER 81-014/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-015-03, /03L-0:on 810728,during Routine Operation,Steam Generator Blowdown Containment Isolation Valve MO-2813 Failed in Open Position.Cause Attributed to Valve Operator Motor Failure.Motor Replaced | /03L-0:on 810728,during Routine Operation,Steam Generator Blowdown Containment Isolation Valve MO-2813 Failed in Open Position.Cause Attributed to Valve Operator Motor Failure.Motor Replaced | | | 05000344/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-016-03, /03L-0:on 810728,during Operator Insp W/Reactor at 80% Power,Train B Hydrogen Recombiner Was Inoperable.Caused by Inadvertent Activation of Fire Protection Deluge Sys. Control Power Transformer Replaced | /03L-0:on 810728,during Operator Insp W/Reactor at 80% Power,Train B Hydrogen Recombiner Was Inoperable.Caused by Inadvertent Activation of Fire Protection Deluge Sys. Control Power Transformer Replaced | | | 05000344/LER-1981-016, Forwards LER 81-016/03L-0.Detailed Event Analysis Encl | Forwards LER 81-016/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-017-03, /03L-0:on 810731,after Increasing Level in C SI Accumulator by 11%,boron Concentration Not Verified within 6-h,per Tech Spec.Caused by Personnel Error.Sample Taken Upon Discovery.Importance of Sample Stressed to Personnel | /03L-0:on 810731,after Increasing Level in C SI Accumulator by 11%,boron Concentration Not Verified within 6-h,per Tech Spec.Caused by Personnel Error.Sample Taken Upon Discovery.Importance of Sample Stressed to Personnel | | | 05000344/LER-1981-018-03, /03L-0:on 810805,turbine First Stage Pressure Channel 506 Found Exceeding Limiting Setting.Caused by Instrument Drift.Instrument Recalibr | /03L-0:on 810805,turbine First Stage Pressure Channel 506 Found Exceeding Limiting Setting.Caused by Instrument Drift.Instrument Recalibr | | | 05000344/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-019-03, /03L-0:on 810902,control Room Emergency Ventilation Humidistat Preheat Coil Would Not Energize to Maintain Control Room Humidity.Caused by Failure of Diaphragm in Humidistat Pneumatic Drive Mechanism | /03L-0:on 810902,control Room Emergency Ventilation Humidistat Preheat Coil Would Not Energize to Maintain Control Room Humidity.Caused by Failure of Diaphragm in Humidistat Pneumatic Drive Mechanism | | | 05000344/LER-1981-020-03, /03L-0:on 810906,during Routine Shift Tour,Train B Control Room Chlorine Detector Inoperative.Caused by Binding Due to Dirty Pump Motor Bearing.Bearing Lubricated, Metering Tube Cleaned & Detector Calibr | /03L-0:on 810906,during Routine Shift Tour,Train B Control Room Chlorine Detector Inoperative.Caused by Binding Due to Dirty Pump Motor Bearing.Bearing Lubricated, Metering Tube Cleaned & Detector Calibr | | | 05000344/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-021-03, /03L-0:on 810910,inadequate Ventilation Found for Train a Preferred Instrument & Control Power Buses.Caused by Insufficient ESF Ventilation Due to Fire Barriers Between a & B Trains.Room Ventilation Will Be Upgraded | /03L-0:on 810910,inadequate Ventilation Found for Train a Preferred Instrument & Control Power Buses.Caused by Insufficient ESF Ventilation Due to Fire Barriers Between a & B Trains.Room Ventilation Will Be Upgraded | | | 05000344/LER-1981-022-03, /03L-0:on 810917,train a Was Inoperable Due to Suction Path from Control Room Being Isolated by Closed Manual Inlet Damper on Ventilation Sys.Caused by Loose Set Screw Allowing Operator to Be Moved W/O Moving Damper | /03L-0:on 810917,train a Was Inoperable Due to Suction Path from Control Room Being Isolated by Closed Manual Inlet Damper on Ventilation Sys.Caused by Loose Set Screw Allowing Operator to Be Moved W/O Moving Damper | | | 05000344/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-023-03, /03L-0:on 810922,during Normal Operation, Containment Atmosphere Sample Return Valve Closed in 10.8-s. Cause Undetermined.Alara Guidelines Restrict Valve Access for Insp During Operation.Insp at Next Refueling Outage | /03L-0:on 810922,during Normal Operation, Containment Atmosphere Sample Return Valve Closed in 10.8-s. Cause Undetermined.Alara Guidelines Restrict Valve Access for Insp During Operation.Insp at Next Refueling Outage | | | 05000344/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-024-03, /03L-0:on 811003,emergency Diesel Generator Declared Inoperable Due to Blown Fuse & Loss of Dc Power. Caused by Failure of Indicator Lamp Socket.Lamp Socket & Dc Fuse Replaced | /03L-0:on 811003,emergency Diesel Generator Declared Inoperable Due to Blown Fuse & Loss of Dc Power. Caused by Failure of Indicator Lamp Socket.Lamp Socket & Dc Fuse Replaced | | | 05000344/LER-1981-025, Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | | | 05000344/LER-1981-025-03, /03L-0:on 811104,power to Preferred Instrument Bus Y11 Lost for 1 Minute Due to Failure of Output Current Sensing Relay on Associated Static Inverter.Caused by Normal Relay end-of-life.Relay Replaced | /03L-0:on 811104,power to Preferred Instrument Bus Y11 Lost for 1 Minute Due to Failure of Output Current Sensing Relay on Associated Static Inverter.Caused by Normal Relay end-of-life.Relay Replaced | | | 05000344/LER-1981-026, Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | Forwards LER 81-026/03L-0.Detailed Event Analysis Encl | |
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