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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                            NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                            REGION III
REGION III  
                                2443 WARRENVILLE ROAD, SUITE 210
2443 WARRENVILLE ROAD, SUITE 210  
                                        LISLE, IL 60532-4352
LISLE, IL 60532-4352  
                                        February 10, 2010
EA-06-178
Mr. Larry Meyer
February 10, 2010  
Site Vice-President
NextEra Energy Point Beach, LLC
6610 Nuclear Road
EA-06-178  
Two Rivers, WI 54241
SUBJECT:         POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED
Mr. Larry Meyer  
                INSPECTION REPORT 05000266/2009005; 05000301/2009005 AND STATUS
Site Vice-President  
                OF CONFIRMATORY ORDER EA-06-178
NextEra Energy Point Beach, LLC  
Dear Mr. Meyer:
6610 Nuclear Road  
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline
Two Rivers, WI 54241  
inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed report documents
the inspection results, which were discussed on January 6, 2010, with Mr. C. Trezise and
SUBJECT:  
members of your staff. The report also documents the status of Confirmatory Order EA-06-178,
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED  
as it relates to your Point Beach Nuclear Plant.
INSPECTION REPORT 05000266/2009005; 05000301/2009005 AND STATUS  
The inspection examined activities conducted under your license as they relate to safety and
OF CONFIRMATORY ORDER EA-06-178  
compliance with the Commission's rules and regulations, and with the conditions of your
Dear Mr. Meyer:  
license. The inspectors reviewed selected procedures and records, observed activities, and
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline  
interviewed your personnel.
inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed report documents  
Based on the results of this inspection, two NRC-identified and three self-revealed findings of
the inspection results, which were discussed on January 6, 2010, with Mr. C. Trezise and  
very low safety significance were identified. Of these findings, four involved a violation of
members of your staff. The report also documents the status of Confirmatory Order EA-06-178,  
NRC requirements. However, because of their very low safety significance, and because the
as it relates to your Point Beach Nuclear Plant.  
issues were entered into your corrective action program, the NRC is treating these issues as
The inspection examined activities conducted under your license as they relate to safety and  
Non-Cited Violations (NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy.
compliance with the Commission's rules and regulations, and with the conditions of your  
If you contest the subject or severity of these NCVs, you should provide a response within
license. The inspectors reviewed selected procedures and records, observed activities, and  
30 days of the date of this Inspection Report, with the basis for your denial, to the U.S. Nuclear
interviewed your personnel.  
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001,
Based on the results of this inspection, two NRC-identified and three self-revealed findings of  
with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
very low safety significance were identified. Of these findings, four involved a violation of  
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
NRC requirements. However, because of their very low safety significance, and because the  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
issues were entered into your corrective action program, the NRC is treating these issues as  
Office at the Point Beach Nuclear Plant. In addition, if you disagree with the characterization of
Non-Cited Violations (NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy.  
any finding in this report, you should provide a response within 30 days of the date of this
If you contest the subject or severity of these NCVs, you should provide a response within  
inspection report, with the basis for your disagreement, to the Regional Administrator,
30 days of the date of this Inspection Report, with the basis for your denial, to the U.S. Nuclear  
Region III, and the NRC Resident Inspector Office at the Point Beach Nuclear Plant.
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001,  
The information that you provide will be considered in accordance with Inspection Manual
with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,  
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector  
Office at the Point Beach Nuclear Plant. In addition, if you disagree with the characterization of  
any finding in this report, you should provide a response within 30 days of the date of this  
inspection report, with the basis for your disagreement, to the Regional Administrator,  
Region III, and the NRC Resident Inspector Office at the Point Beach Nuclear Plant.
The information that you provide will be considered in accordance with Inspection Manual  
Chapter 0305.
Chapter 0305.


L. Meyer                                       -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document
L. Meyer  
Room or from the Publicly Available Records System (PARS) component of NRC's document
system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-
rm/adams.html (the Public Electronic Reading Room).
                                              Sincerely,
                                              /RA/
-2-  
                                              Michael Kunowski, Chief
                                              Branch 5
                                              Division of Reactor Projects
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its  
Docket Nos. 50-266; 50-301
enclosure will be available electronically for public inspection in the NRC Public Document  
License Nos. DPR-24; DPR-27
Room or from the Publicly Available Records System (PARS) component of NRC's document  
Enclosure:     IR 05000266/2009005; 05000301/2009005
system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-
                w/Attachment: Supplemental Information
rm/adams.html (the Public Electronic Reading Room).  
cc w/encl:     Distribution via ListServe
Sincerely,  
/RA/  
Michael Kunowski, Chief  
Branch 5  
Division of Reactor Projects  
Docket Nos. 50-266; 50-301  
License Nos. DPR-24; DPR-27  
Enclosure:  
IR 05000266/2009005; 05000301/2009005
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServe  


          U.S. NUCLEAR REGULATORY COMMISSION
                          REGION III
Enclosure
Docket Nos:         50-266; 50-301
U.S. NUCLEAR REGULATORY COMMISSION  
License Nos:       DPR-24; DPR-27
REGION III  
Report No:         05000266/2009005; 05000301/2009005
Docket Nos:  
Licensee:           NextEra Energy Point Beach, LLC
50-266; 50-301  
Facility:           Point Beach Nuclear Plant, Units 1 and 2
License Nos:  
Location:           Two Rivers, WI
DPR-24; DPR-27  
Dates:             October 1, 2009, through December 31, 2009
Report No:  
Inspectors:         S. Burton, Senior Resident Inspector
05000266/2009005; 05000301/2009005
                    R. Ruiz, Senior Resident Inspector (Acting)
Licensee:  
                    M. Thorpe-Kavanaugh, Resident Inspector (Acting)
NextEra Energy Point Beach, LLC  
                    J. Jandovitz, Project Engineer
Facility:  
                    J. Cassidy, Senior Health Physicist
Point Beach Nuclear Plant, Units 1 and 2  
`                   R. Jickling, Senior Emergency Preparedness Inspector
Location:  
                    D. Jones, Reactor Inspector
Two Rivers, WI  
                    D. McNeil, Senior Operations Engineer
Dates:  
                    R. Edwards, Reactor Engineer
October 1, 2009, through December 31, 2009  
                    J. Gilliam, Reactor Engineer
Inspectors:  
                    E. Sanchez-Santiago, Reactor Engineer
S. Burton, Senior Resident Inspector  
                    N. Feliz Adorno, Reactor Engineer
Approved by:       M. Kunowski, Chief
R. Ruiz, Senior Resident Inspector (Acting)  
                    Branch 5
                    Division of Reactor Projects
M. Thorpe-Kavanaugh, Resident Inspector (Acting)  
                                                                  Enclosure
J. Jandovitz, Project Engineer
J. Cassidy, Senior Health Physicist  
`  
R. Jickling, Senior Emergency Preparedness Inspector  
D. Jones, Reactor Inspector  
D. McNeil, Senior Operations Engineer  
R. Edwards, Reactor Engineer  
J. Gilliam, Reactor Engineer  
E. Sanchez-Santiago, Reactor Engineer  
N. Feliz Adorno, Reactor Engineer  
Approved by:  
M. Kunowski, Chief  
Branch 5  
Division of Reactor Projects


                                        TABLE OF CONTENTS
SUMMARY OF FINDINGS ...........................................................................................................1
Enclosure
REPORT DETAILS .......................................................................................................................5
TABLE OF CONTENTS  
Summary of Plant Status...........................................................................................................5
SUMMARY OF FINDINGS ...........................................................................................................1  
  1.   REACTOR SAFETY .......................................................................................................5
REPORT DETAILS.......................................................................................................................5  
      1R01     Adverse Weather Protection (71111.01) .............................................................5
Summary of Plant Status...........................................................................................................5  
      1R04     Equipment Alignment (71111.04) ........................................................................5
1.  
      1R05     Fire Protection (71111.05) ...................................................................................7
REACTOR SAFETY .......................................................................................................5  
      1R06     Flooding (71111.06).............................................................................................8
1R01  
      1R08     Inservice Inspection (ISI) Activities (71111.08P) .................................................8
Adverse Weather Protection (71111.01) .............................................................5  
      1R11     Licensed Operator Requalification Program (71111.11)....................................11
1R04  
      1R12     Maintenance Effectiveness (71111.12) .............................................................13
Equipment Alignment (71111.04) ........................................................................5  
      1R13     Maintenance Risk Assessments and Emergent Work Control (71111.13) ........16
1R05  
      1R15     Operability Evaluations (71111.15)....................................................................16
Fire Protection (71111.05) ...................................................................................7  
      1R18     Plant Modifications (71111.18) ..........................................................................20
1R06  
      1R19     Post-Maintenance Testing (71111.19)...............................................................25
Flooding (71111.06).............................................................................................8  
      1R20     Outage Activities (71111.20) .............................................................................26
1R08  
      1R22     Surveillance Testing (71111.22) ........................................................................29
Inservice Inspection (ISI) Activities (71111.08P) .................................................8  
      1EP2     Alert and Notification System (ANS) Evaluation (71114.02)..............................30
1R11  
      1EP3     Emergency Response Organization Augmentation Testing (71114.03)............30
Licensed Operator Requalification Program (71111.11)....................................11  
      1EP4     Emergency Action Level and Emergency Plan Changes (71114.04) ................31
1R12  
      1EP5     Correction of EP Weaknesses and Deficiencies (71114.05) .............................31
Maintenance Effectiveness (71111.12) .............................................................13  
  2.   RADIATION SAFETY ...................................................................................................32
1R13
      2OS1 Access Control to Radiologically Significant Areas (71121.01) .........................32
Maintenance Risk Assessments and Emergent Work Control (71111.13)........16  
      2OS2 ALARA Planning and Controls (71121.02) ........................................................37
1R15  
  4.   OTHER ACTIVITIES ....................................................................................................38
Operability Evaluations (71111.15)....................................................................16  
      4OA1 PI Verification (71151) .......................................................................................38
1R18  
      4OA2 Identification and Resolution of Problems (71152) ............................................41
Plant Modifications (71111.18) ..........................................................................20  
      4OA5 Other Activities...................................................................................................43
1R19  
      4OA6 Management Meetings ......................................................................................53
Post-Maintenance Testing (71111.19)...............................................................25  
SUPPLEMENTAL INFORMATION ...............................................................................................1
1R20  
Key Points of Contact................................................................................................................1
Outage Activities (71111.20) .............................................................................26  
List of Items Opened, Closed and Discussed ...........................................................................1
1R22  
List of Documents Reviewed .....................................................................................................3
Surveillance Testing (71111.22) ........................................................................29  
List of Acronyms Used ............................................................................................................18
1EP2  
                                                                                                                        Enclosure
Alert and Notification System (ANS) Evaluation (71114.02)..............................30  
1EP3  
Emergency Response Organization Augmentation Testing (71114.03)............30  
1EP4  
Emergency Action Level and Emergency Plan Changes (71114.04)................31  
1EP5  
Correction of EP Weaknesses and Deficiencies (71114.05) .............................31  
2.  
RADIATION SAFETY ...................................................................................................32  
2OS1  
Access Control to Radiologically Significant Areas (71121.01) .........................32  
2OS2  
ALARA Planning and Controls (71121.02) ........................................................37  
4.  
OTHER ACTIVITIES ....................................................................................................38  
4OA1  
PI Verification (71151) .......................................................................................38  
4OA2  
Identification and Resolution of Problems (71152) ............................................41  
4OA5  
Other Activities...................................................................................................43  
4OA6
Management Meetings ......................................................................................53  
SUPPLEMENTAL INFORMATION ...............................................................................................1  
Key Points of Contact................................................................................................................1  
List of Items Opened, Closed and Discussed ...........................................................................1  
List of Documents Reviewed.....................................................................................................3  
List of Acronyms Used ............................................................................................................18  


                                    SUMMARY OF FINDINGS
IR 05000266/2009005, 05000301/2009005; 10/01/2009 - 12/31/2009; Point Beach Nuclear
Enclosure
Plant, Units 1 & 2; Maintenance Effectiveness, Operability Evaluations, Plant Modifications,
1
Outage Activities, and Other Activities.
SUMMARY OF FINDINGS  
This report covers a three-month period of inspection by resident inspectors and announced
IR 05000266/2009005, 05000301/2009005; 10/01/2009 - 12/31/2009; Point Beach Nuclear  
baseline inspections by regional inspectors. Also discussed is the status of Confirmatory Order
Plant, Units 1 & 2; Maintenance Effectiveness, Operability Evaluations, Plant Modifications,  
EA-06-178. Five Green findings were either self-revealed or identified by inspectors in this
Outage Activities, and Other Activities.  
inspection period. Four of the findings had associated Non-Cited Violations of
This report covers a three-month period of inspection by resident inspectors and announced  
NRC requirements, and one finding had no associated violation of regulatory requirements.
baseline inspections by regional inspectors. Also discussed is the status of Confirmatory Order  
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
EA-06-178. Five Green findings were either self-revealed or identified by inspectors in this  
Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP).
inspection period. Four of the findings had associated Non-Cited Violations of  
Findings for which the SDP does not apply may be Green or be assigned a severity level after
NRC requirements, and one finding had no associated violation of regulatory requirements.
NRC management review. The NRC's program for overseeing the safe operation of commercial
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using  
nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,
Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP).
dated December 2006.
Findings for which the SDP does not apply may be Green or be assigned a severity level after  
A.     NRC-Identified and Self-Revealed Findings
NRC management review. The NRC's program for overseeing the safe operation of commercial  
        Cornerstone: Mitigating Systems
nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,  
    *   Green. The inspectors identified a finding of very low safety significance for the failure to
dated December 2006.  
        meet a commitment made in the Generic Letter (GL) 89-13 program. Specifically, the
A.  
        program states that biocide treatments at Point Beach are performed at least annually
NRC-Identified and Self-Revealed Findings  
        and are directly applied to the service water system for mussel control and eradication to
Cornerstone: Mitigating Systems  
        prevent fouling of safety-related heat exchangers. However, the 2008 biocide treatment
*  
        for mussel control was deferred until 2009. After the treatment in 2009, greater than
Green. The inspectors identified a finding of very low safety significance for the failure to  
        expected tube blockage and reduced flow to safety-related heat exchangers due to
meet a commitment made in the Generic Letter (GL) 89-13 program. Specifically, the  
        mussels was identified. In response, the licensee adjusted flow through the affected
program states that biocide treatments at Point Beach are performed at least annually  
        heat exchangers and opened and cleaned the heat exchangers to remove mussels that
and are directly applied to the service water system for mussel control and eradication to  
        caused the tube blockage. The licensee took corrective actions to ensure that future
prevent fouling of safety-related heat exchangers. However, the 2008 biocide treatment  
        annual biocide treatments would be conducted annually.
for mussel control was deferred until 2009. After the treatment in 2009, greater than  
        This finding was more than minor because it was associated with the equipment
expected tube blockage and reduced flow to safety-related heat exchangers due to  
        performance attribute of the Mitigating Systems Cornerstone and adversely affected the
mussels was identified. In response, the licensee adjusted flow through the affected  
        associated cornerstone objective of ensuring the availability, reliability, and capability of
heat exchangers and opened and cleaned the heat exchangers to remove mussels that  
        systems that respond to initiating events to prevent undesirable consequences. The
caused the tube blockage. The licensee took corrective actions to ensure that future  
        inspectors determined the finding could be evaluated using the SDP in accordance with
annual biocide treatments would be conducted annually.  
        IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial
This finding was more than minor because it was associated with the equipment  
        Screening and Characterization of Findings," Table 4a, for the Mitigating Systems
performance attribute of the Mitigating Systems Cornerstone and adversely affected the  
        Cornerstone, dated January 10, 2008. The finding was determined to be of very low
associated cornerstone objective of ensuring the availability, reliability, and capability of  
        safety significance because the issue did not result in the actual loss of a safety function.
systems that respond to initiating events to prevent undesirable consequences. The  
        This finding did not involve a violation of NRC regulatory requirements. The inspectors
inspectors determined the finding could be evaluated using the SDP in accordance with  
        determined this performance deficiency was not indicative of current performance;
IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial  
        therefore, no cross-cutting aspect was identified. (Section 1R12.1)
Screening and Characterization of Findings," Table 4a, for the Mitigating Systems  
    *   Green. The inspectors identified a finding of very low safety significance and associated
Cornerstone, dated January 10, 2008. The finding was determined to be of very low  
        Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the
safety significance because the issue did not result in the actual loss of a safety function.
        failure to update the Safe Load Path Manual for the Unit 2 turbine building (SLP-3) as
This finding did not involve a violation of NRC regulatory requirements. The inspectors  
        part of the mid-1990's modification that added the G-03 and G-04 emergency diesel
determined this performance deficiency was not indicative of current performance;  
                                                  1                                      Enclosure
therefore, no cross-cutting aspect was identified. (Section 1R12.1)  
*  
Green. The inspectors identified a finding of very low safety significance and associated  
Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the  
failure to update the Safe Load Path Manual for the Unit 2 turbine building (SLP-3) as  
part of the mid-1990's modification that added the G-03 and G-04 emergency diesel  


  generators. Specifically, it was identified that SLP-3 allowed unrestricted load lifts over
  the Unit 2 turbine building truck bay area based upon a 1980's evaluation, and was not
Enclosure
  updated to reflect a modification that added safety-related cables for emergency diesel
2
  generators under the Unit 2 truck bay. Due to the close proximity of the A train cables
generators. Specifically, it was identified that SLP-3 allowed unrestricted load lifts over  
  to the B train cables, a loss of both trains of emergency alternating current (AC) power
the Unit 2 turbine building truck bay area based upon a 1980's evaluation, and was not  
  could result if the underground cables were disabled by a dropped load of sufficient
updated to reflect a modification that added safety-related cables for emergency diesel  
  magnitude. The licensee addressed the immediate concern by installing temporary steel
generators under the Unit 2 truck bay. Due to the close proximity of the A train cables  
  plates over the affected area of the truck bay to provide adequate protection for
to the B train cables, a loss of both trains of emergency alternating current (AC) power  
  upcoming heavy load lifts. Additionally, the licensee revised SLP-3 to require additional
could result if the underground cables were disabled by a dropped load of sufficient  
  risk mitigation measures be taken prior to heavy load lifts in that area.
magnitude. The licensee addressed the immediate concern by installing temporary steel  
  The finding was more than minor because it was associated with the Mitigating Systems
plates over the affected area of the truck bay to provide adequate protection for  
  Cornerstone attribute of design control and adversely affected the associated
upcoming heavy load lifts. Additionally, the licensee revised SLP-3 to require additional  
  cornerstone objective of ensuring the availability, reliability, and capability of systems
risk mitigation measures be taken prior to heavy load lifts in that area.  
  that respond to initiating events to prevent undesirable consequences
The finding was more than minor because it was associated with the Mitigating Systems  
  (i.e., core damage). The inspectors determined the finding could be evaluated using
Cornerstone attribute of design control and adversely affected the associated  
  the SDP in accordance with IMC 0609, "Significance Determination Process,"
cornerstone objective of ensuring the availability, reliability, and capability of systems  
  Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings,"
that respond to initiating events to prevent undesirable consequences  
  Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008. The finding
(i.e., core damage). The inspectors determined the finding could be evaluated using  
  was determined to be of very low safety significance because the issue did not result in
the SDP in accordance with IMC 0609, "Significance Determination Process,"  
  the actual loss of a safety function. This finding had a cross-cutting aspect in the area of
Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings,"  
  problem identification and resolution, corrective action program component, because the
Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008. The finding  
  staff did not take appropriate corrective actions to address safety issues in a timely
was determined to be of very low safety significance because the issue did not result in  
  manner, commensurate with their safety significance. Specifically, in 2008, when
the actual loss of a safety function. This finding had a cross-cutting aspect in the area of  
  questions were raised by licensee staff regarding the adequacy of SLP-3, the SLP was
problem identification and resolution, corrective action program component, because the  
  not revised (P.1(d)). (Section 1R18.1)
staff did not take appropriate corrective actions to address safety issues in a timely  
* Green. A self-revealed finding of very low safety significance and associated Non-Cited
manner, commensurate with their safety significance. Specifically, in 2008, when  
  Violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and
questions were raised by licensee staff regarding the adequacy of SLP-3, the SLP was  
  Drawings," was identified for performing an Instrumentation and Control (I&C) procedure
not revised (P.1(d)). (Section 1R18.1)  
  that was inappropriate to the circumstances, and resulted in the momentary loss of all
*  
  available channels of reactor vessel level indication in the control room. As part of the
Green. A self-revealed finding of very low safety significance and associated Non-Cited  
  immediate corrective actions, the licensee suspended the performance of the procedure
Violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and  
  and sent an operator into containment to verify reactor vessel level via the local
Drawings," was identified for performing an Instrumentation and Control (I&C) procedure  
  standpipe level indicator and to ensure level indication was reestablished. Additionally,
that was inappropriate to the circumstances, and resulted in the momentary loss of all  
  the licensee applied a work planning logic-tie to this activity to ensure the reactor was
available channels of reactor vessel level indication in the control room. As part of the  
  de-fueled prior to performing this calibration and was currently evaluating the need for
immediate corrective actions, the licensee suspended the performance of the procedure  
  revisions to the procedure.
and sent an operator into containment to verify reactor vessel level via the local  
  The finding was more than minor because it was associated with the Mitigating Systems
standpipe level indicator and to ensure level indication was reestablished. Additionally,  
  Cornerstone attribute of procedure quality and adversely affected the associated
the licensee applied a work planning logic-tie to this activity to ensure the reactor was  
  cornerstone objective to ensure the availability, reliability, and capability of systems that
de-fueled prior to performing this calibration and was currently evaluating the need for  
  respond to initiating events to prevent undesirable consequences (i.e., core damage).
revisions to the procedure.  
  The inspectors assessed the significance of the finding in accordance with IMC 0609,
The finding was more than minor because it was associated with the Mitigating Systems  
  Appendix G, "Shutdown Operations Significance Determination Process," and
Cornerstone attribute of procedure quality and adversely affected the associated  
  determined that this issue required a Phase 2 analysis since the finding increased the
cornerstone objective to ensure the availability, reliability, and capability of systems that  
  likelihood of a loss of reactor coolant system inventory. The inspectors and a senior
respond to initiating events to prevent undesirable consequences (i.e., core damage).
  reactor analyst determined through the analysis that this issue is best characterized as a
The inspectors assessed the significance of the finding in accordance with IMC 0609,  
  finding of very low safety significance. This finding had a cross-cutting aspect in the
Appendix G, "Shutdown Operations Significance Determination Process," and  
  area of human performance, work control component, in that the licensee did not
determined that this issue required a Phase 2 analysis since the finding increased the  
  appropriately coordinate work activities for the existing plant conditions to ensure the
likelihood of a loss of reactor coolant system inventory. The inspectors and a senior  
                                              2                                        Enclosure
reactor analyst determined through the analysis that this issue is best characterized as a  
finding of very low safety significance. This finding had a cross-cutting aspect in the  
area of human performance, work control component, in that the licensee did not  
appropriately coordinate work activities for the existing plant conditions to ensure the  


  operational impact on reactor vessel level indication while at a water level above
  reduced inventory was fully understood (H.3(b)). (Section 1R20.1)
Enclosure
  Cornerstone: Barrier Integrity
3
* Green. A self-revealed finding of very low safety significance and associated Non-Cited
operational impact on reactor vessel level indication while at a water level above  
  Violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and
reduced inventory was fully understood (H.3(b)). (Section 1R20.1)  
  Drawings," was identified for the failure to ensure adequate control of foreign material in
Cornerstone: Barrier Integrity  
  accordance with the requirements of procedure NP 8.4.10, "Exclusion of Foreign
*  
  Material from Plant Components and Systems." Specifically, on October 17, 2009,
Green. A self-revealed finding of very low safety significance and associated Non-Cited  
  foreign material was discovered inside the 2SI-897B valve after the valve failed to
Violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and  
  properly stroke during the performance of procedure IT-215, "SI Valves -
Drawings," was identified for the failure to ensure adequate control of foreign material in  
  Cold Shutdown." The licensee took prompt corrective actions to repair the valve and
accordance with the requirements of procedure NP 8.4.10, "Exclusion of Foreign  
  perform an extent-of-condition review. Additionally, upon entering the issue into its
Material from Plant Components and Systems." Specifically, on October 17, 2009,  
  corrective action program, the licensee performed a causal evaluation to determine any
foreign material was discovered inside the 2SI-897B valve after the valve failed to  
  additional corrective actions.
properly stroke during the performance of procedure IT-215, "SI Valves -  
  The finding was more than minor because it was associated with the Barrier Integrity
Cold Shutdown." The licensee took prompt corrective actions to repair the valve and  
  Cornerstone attribute of human performance and adversely affected the associated
perform an extent-of-condition review. Additionally, upon entering the issue into its  
  cornerstone objective of providing reasonable assurance that physical design barriers
corrective action program, the licensee performed a causal evaluation to determine any  
  protect the public from radionuclide releases caused by accidents or events.
additional corrective actions.  
  Specifically, due to the interference caused by the foreign material inside the 2SI-897B
The finding was more than minor because it was associated with the Barrier Integrity  
  valve, the valve would not have been able to perform its safety function to close during
Cornerstone attribute of human performance and adversely affected the associated  
  the initiation of the post-LOCA (loss of coolant accident) sump-recirculation phase of
cornerstone objective of providing reasonable assurance that physical design barriers  
  safety injection. The inspectors determined the finding could be evaluated in
protect the public from radionuclide releases caused by accidents or events.
  accordance with IMC 0609, Significance Determination Process," Attachment 0609.04,
Specifically, due to the interference caused by the foreign material inside the 2SI-897B  
  Phase 1 - Initial Screening and Characterization of Findings," Table 4a, dated
valve, the valve would not have been able to perform its safety function to close during  
  January 10, 2008. The finding was determined to be of very low safety significance
the initiation of the post-LOCA (loss of coolant accident) sump-recirculation phase of  
  because the issue did not represent a degradation of the radiological barrier function
safety injection. The inspectors determined the finding could be evaluated in  
  provided for the control room, the auxiliary building, or the spent fuel pool; represent a
accordance with IMC 0609, Significance Determination Process," Attachment 0609.04,  
  degradation of the barrier function of the control room against smoke or a toxic
Phase 1 - Initial Screening and Characterization of Findings," Table 4a, dated  
  atmosphere; represent an actual open pathway in the physical integrity of reactor
January 10, 2008. The finding was determined to be of very low safety significance  
  containment (valves, airlocks, containment isolation system (logic and instrumentation)),
because the issue did not represent a degradation of the radiological barrier function  
  and heat removal components; or involve an actual reduction in function of hydrogen
provided for the control room, the auxiliary building, or the spent fuel pool; represent a  
  ignitors in the reactor containment. No cross-cutting aspect was identified because the
degradation of the barrier function of the control room against smoke or a toxic  
  foreign material was determined to have been introduced into the system in the past and
atmosphere; represent an actual open pathway in the physical integrity of reactor  
  was not considered indicative of current performance. (Section 1R15.1)
containment (valves, airlocks, containment isolation system (logic and instrumentation)),  
  Cornerstone: Public Radiation Safety
and heat removal components; or involve an actual reduction in function of hydrogen  
* Green. A self-revealed finding of very low safety significance and associated Non-Cited
ignitors in the reactor containment. No cross-cutting aspect was identified because the  
  Violation of 10 CFR 20.1101(b) was identified for the failure to adequately control
foreign material was determined to have been introduced into the system in the past and  
  radioactive material to prevent its migration outside the radiologically controlled area
was not considered indicative of current performance. (Section 1R15.1)  
  (RCA), as required by licensee procedures. On May 21, 2009, a contract worker
Cornerstone: Public Radiation Safety  
  performing inspections of the main electrical transformers located outside the RCA
*  
  picked-up a wadded-ball of debris (unmarked tape) and placed it in his front pants
Green. A self-revealed finding of very low safety significance and associated Non-Cited  
  pocket. The debris was later found to be radioactively contaminated when the worker
Violation of 10 CFR 20.1101(b) was identified for the failure to adequately control  
  alarmed the protected area exit radiation monitors a few hours later as he attempted to
radioactive material to prevent its migration outside the radiologically controlled area  
  leave the site. The tape was likely used to cover contaminated hoses that were
(RCA), as required by licensee procedures. On May 21, 2009, a contract worker  
  previously used within the Point Beach RCA, but had escaped the licensee's control and
performing inspections of the main electrical transformers located outside the RCA  
  migrated (blew) into the transformer area outdoors where it was found by the worker.
picked-up a wadded-ball of debris (unmarked tape) and placed it in his front pants  
                                            3                                      Enclosure
pocket. The debris was later found to be radioactively contaminated when the worker  
alarmed the protected area exit radiation monitors a few hours later as he attempted to  
leave the site. The tape was likely used to cover contaminated hoses that were  
previously used within the Point Beach RCA, but had escaped the licensee's control and  
migrated (blew) into the transformer area outdoors where it was found by the worker.


  The licensee's storage of radioactive material in an outdoor satellite RCA and/or the
  licensee's radioactive material control practices during refueling outages when the
Enclosure
  containment building equipment hatch was open to the environment led to the escape of
4
  the material outside the RCA. The contractor's assigned work duties should not have
The licensee's storage of radioactive material in an outdoor satellite RCA and/or the  
  involved exposure to radioactive material; consequently, the worker was unnecessarily
licensee's radioactive material control practices during refueling outages when the  
  exposed to radiation from the contaminated tape. A dose evaluation completed by the
containment building equipment hatch was open to the environment led to the escape of  
  licensee's consultant determined that the effective dose equivalent to the worker's thigh
the material outside the RCA. The contractor's assigned work duties should not have  
  from exposure to the contaminated ball of tape was approximately one mrem.
involved exposure to radioactive material; consequently, the worker was unnecessarily  
  The licensee's corrective action called for expanded radiation protection oversight during
exposed to radiation from the contaminated tape. A dose evaluation completed by the  
  movement of material in outdoor areas. Procedures were revised to include a
licensee's consultant determined that the effective dose equivalent to the worker's thigh  
  post-outage walkdown of outdoor areas near the RCA yard. Additionally, the licensee
from exposure to the contaminated ball of tape was approximately one mrem.
  planned to construct an enclosure so that storage/transfer of contaminated materials
The licensee's corrective action called for expanded radiation protection oversight during  
  could be performed indoors.
movement of material in outdoor areas. Procedures were revised to include a  
  The finding was more than minor because it impacted the program and process attribute
post-outage walkdown of outdoor areas near the RCA yard. Additionally, the licensee  
  of the Public Radiation Safety Cornerstone and adversely affected the cornerstone
planned to construct an enclosure so that storage/transfer of contaminated materials  
  objective of ensuring adequate protection of public health and safety from exposure to
could be performed indoors.  
  radiation, in that, unnecessary radiation exposure was received by an individual from
The finding was more than minor because it impacted the program and process attribute  
  inadequately controlled radioactive material. The finding was determined to be of very
of the Public Radiation Safety Cornerstone and adversely affected the cornerstone  
  low safety significance because: (1) it involved a radioactive material control problem
objective of ensuring adequate protection of public health and safety from exposure to  
  that was contrary to NRC requirements and the licensee's procedure; and (2) the dose
radiation, in that, unnecessary radiation exposure was received by an individual from  
  impact to a member of the public (the contract worker) within the licensee's restricted
inadequately controlled radioactive material. The finding was determined to be of very  
  area was less than 5 millirem total effective dose equivalent. The cause of the
low safety significance because: (1) it involved a radioactive material control problem  
  radioactive material control problem involved a cross-cutting component in the human
that was contrary to NRC requirements and the licensee's procedure; and (2) the dose  
  performance area for inadequate work control, in that, job site conditions including
impact to a member of the public (the contract worker) within the licensee's restricted  
  environmental conditions (high winds, night time work, etc.) impacted human
area was less than 5 millirem total effective dose equivalent. The cause of the  
  performance and consequently, radiological safety, during movement of
radioactive material control problem involved a cross-cutting component in the human  
  material/equipment in outdoor areas (H.3.(a)). (Section 4OA5.1)
performance area for inadequate work control, in that, job site conditions including  
B. Licensee-Identified Violations
environmental conditions (high winds, night time work, etc.) impacted human  
  None.
performance and consequently, radiological safety, during movement of  
                                            4                                      Enclosure
material/equipment in outdoor areas (H.3.(a)). (Section 4OA5.1)  
B.  
Licensee-Identified Violations  
None.  


                                        REPORT DETAILS
Summary of Plant Status
Enclosure
Unit 1 was at 100 percent power throughout the entire inspection period with the exception of a
5
planned reduction in power during routine auxiliary feedwater (AFW) testing and an unplanned
REPORT DETAILS  
down-power to approximately 45 percent power on November 17, 2009, due to a lake grass
Summary of Plant Status  
influx and subsequent condenser cleaning evolution.
Unit 1 was at 100 percent power throughout the entire inspection period with the exception of a  
Unit 2 was at 100 percent power at the beginning of the inspection period, shut down to
planned reduction in power during routine auxiliary feedwater (AFW) testing and an unplanned  
commence a refueling outage (U2R30) on October 15, 2009, restarted on December 5, and
down-power to approximately 45 percent power on November 17, 2009, due to a lake grass  
returned to 100 percent power on December 11. Unit 2 remained at or near 100 percent power
influx and subsequent condenser cleaning evolution.  
for the remainder of the inspection period.
Unit 2 was at 100 percent power at the beginning of the inspection period, shut down to  
1.     REACTOR SAFETY
commence a refueling outage (U2R30) on October 15, 2009, restarted on December 5, and  
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
returned to 100 percent power on December 11. Unit 2 remained at or near 100 percent power  
1R01 Adverse Weather Protection (71111.01)
for the remainder of the inspection period.  
  .1   Winter Seasonal Readiness Preparations
1.  
    a. Inspection Scope
REACTOR SAFETY  
        The inspectors conducted a review of the licensees preparations for winter to verify that
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
        the plants design features and implementation of procedures were sufficient to protect
1R01 Adverse Weather Protection (71111.01)  
        mitigating systems from the effects of adverse weather. The inspectors walked down
.1  
        accessible portions of risk-significant equipment and systems susceptible to cold
Winter Seasonal Readiness Preparations  
        weather freezing prior to the onset of severe cold weather. The inspectors walked down
a.  
        all accessible portions of the Units 1 and 2 facade buildings, which enclosed the reactor
Inspection Scope  
        containments, and certain safety-related plant equipment inside the protected area. The
The inspectors conducted a review of the licensees preparations for winter to verify that  
        inspectors reviewed the corrective action documents and work orders (WOs) written for
the plants design features and implementation of procedures were sufficient to protect  
        identified problems. The inspectors also walked down areas that had a history of freeze
mitigating systems from the effects of adverse weather. The inspectors walked down  
        problems to ensure that previous corrective actions were implemented. Documents
accessible portions of risk-significant equipment and systems susceptible to cold  
        reviewed are listed in the Attachment to this report.
weather freezing prior to the onset of severe cold weather. The inspectors walked down  
        This inspection constituted one winter seasonal readiness preparations sample as
all accessible portions of the Units 1 and 2 facade buildings, which enclosed the reactor  
        defined in Inspection Procedure (IP) 71111.01-05.
containments, and certain safety-related plant equipment inside the protected area. The  
    b. Findings
inspectors reviewed the corrective action documents and work orders (WOs) written for  
        No findings of significance were identified.
identified problems. The inspectors also walked down areas that had a history of freeze  
1R04 Equipment Alignment (71111.04)
problems to ensure that previous corrective actions were implemented. Documents  
  .1   Quarterly Partial System Walkdowns
reviewed are listed in the Attachment to this report.  
    a. Inspection Scope
This inspection constituted one winter seasonal readiness preparations sample as  
        The inspectors performed a partial system walkdown of the spent fuel pool cooling
defined in Inspection Procedure (IP) 71111.01-05.  
        system.
b.  
                                                  5                                    Enclosure
Findings  
No findings of significance were identified.  
1R04 Equipment Alignment (71111.04)  
.1  
Quarterly Partial System Walkdowns  
a.  
Inspection Scope  
The inspectors performed a partial system walkdown of the spent fuel pool cooling  
system.  


    The inspectors selected this system based on its risk significance relative to the Reactor
    Safety Cornerstones at the time it was inspected. The inspectors attempted to identify
Enclosure
    any discrepancies that could impact the function of the system, and, therefore,
6
    potentially increase risk. The inspectors reviewed applicable operating procedures,
The inspectors selected this system based on its risk significance relative to the Reactor  
    system diagrams, Final Safety Analysis Report (FSAR), Technical Specification (TS)
Safety Cornerstones at the time it was inspected. The inspectors attempted to identify  
    requirements, outstanding WOs, condition reports, and the impact of ongoing work
any discrepancies that could impact the function of the system, and, therefore,  
    activities on redundant trains of equipment in order to identify conditions that could have
potentially increase risk. The inspectors reviewed applicable operating procedures,  
    rendered the systems incapable of performing their intended functions. The inspectors
system diagrams, Final Safety Analysis Report (FSAR), Technical Specification (TS)  
    also walked down accessible portions of the system to verify system components and
requirements, outstanding WOs, condition reports, and the impact of ongoing work  
    support equipment were aligned correctly and operable. The inspectors examined the
activities on redundant trains of equipment in order to identify conditions that could have  
    material condition of the components and observed operating parameters of equipment
rendered the systems incapable of performing their intended functions. The inspectors  
    to verify that there were no obvious deficiencies. The inspectors also verified that the
also walked down accessible portions of the system to verify system components and  
    licensee had properly identified and resolved equipment alignment problems that could
support equipment were aligned correctly and operable. The inspectors examined the  
    cause initiating events or impact the capability of mitigating systems or barriers and
material condition of the components and observed operating parameters of equipment  
    entered them into the corrective action program (CAP) with the appropriate significance
to verify that there were no obvious deficiencies. The inspectors also verified that the  
    characterization. Documents reviewed are listed in the Attachment to this report.
licensee had properly identified and resolved equipment alignment problems that could  
    These activities constituted one partial system walkdown sample as defined in
cause initiating events or impact the capability of mitigating systems or barriers and  
    IP 71111.04-05.
entered them into the corrective action program (CAP) with the appropriate significance  
  b. Findings
characterization. Documents reviewed are listed in the Attachment to this report.  
    No findings of significance were identified.
These activities constituted one partial system walkdown sample as defined in  
.2   Semi-Annual Complete System Walkdown
IP 71111.04-05.  
  a. Inspection Scope
b.  
    During the Unit 2 refueling outage (U2R30), the inspectors performed a complete system
Findings  
    alignment inspection of the residual heat removal (RHR) system to verify the functional
No findings of significance were identified.  
    capability of the system. This system was selected because it was considered both
.2  
    safety-significant and risk-significant in the licensee's probabilistic risk assessment.
Semi-Annual Complete System Walkdown  
    The inspectors walked down the system to review mechanical and electrical equipment
a.  
    lineups, electrical power availability, system pressure and temperature indications, as
Inspection Scope  
    appropriate, component labeling, component lubrication, component and equipment
During the Unit 2 refueling outage (U2R30), the inspectors performed a complete system  
    cooling, hangers and supports, operability of support systems, and to ensure that
alignment inspection of the residual heat removal (RHR) system to verify the functional  
    ancillary equipment or debris did not interfere with equipment operation. A review of a
capability of the system. This system was selected because it was considered both  
    sample of past and outstanding WOs was performed to determine whether any
safety-significant and risk-significant in the licensee's probabilistic risk assessment.
    deficiencies significantly affected the system function. In addition, the inspectors
The inspectors walked down the system to review mechanical and electrical equipment  
    reviewed the CAP database to ensure that system equipment alignment problems were
lineups, electrical power availability, system pressure and temperature indications, as  
    being identified and appropriately resolved. Documents reviewed are listed in the
appropriate, component labeling, component lubrication, component and equipment  
    Attachment to this report.
cooling, hangers and supports, operability of support systems, and to ensure that  
    These activities constituted one complete system walkdown sample as defined in
ancillary equipment or debris did not interfere with equipment operation. A review of a  
    IP 71111.04-05.
sample of past and outstanding WOs was performed to determine whether any  
  b. Findings
deficiencies significantly affected the system function. In addition, the inspectors  
    No findings of significance were identified.
reviewed the CAP database to ensure that system equipment alignment problems were  
                                                6                                      Enclosure
being identified and appropriately resolved. Documents reviewed are listed in the  
Attachment to this report.  
These activities constituted one complete system walkdown sample as defined in  
IP 71111.04-05.  
b.  
Findings  
No findings of significance were identified.  


1R05 Fire Protection (71111.05)
.1   Routine Resident Inspector Tours (71111.05Q)
Enclosure
  a. Inspection Scope
7
      The inspectors conducted fire protection walkdowns that were focused on availability,
1R05 Fire Protection (71111.05)  
      accessibility, and the condition of firefighting equipment in the following risk-significant
.1  
      plant areas:
Routine Resident Inspector Tours (71111.05Q)  
      *       fire zone 245 - Unit 1 electrical equipment room;
a.  
      *       fire zone 318 - cable spreading room;
Inspection Scope  
      *       fire zone 775 - G-04 emergency diesel generator (EDG); and
The inspectors conducted fire protection walkdowns that were focused on availability,  
      *       fire zone 301 - Unit 2 turbine building basement.
accessibility, and the condition of firefighting equipment in the following risk-significant  
      The inspectors reviewed areas to assess if the licensee had implemented a fire
plant areas:  
      protection program that adequately controlled combustibles and ignition sources within
*  
      the plant, effectively maintained fire detection and suppression capability, maintained
fire zone 245 - Unit 1 electrical equipment room;  
      passive fire protection features in good material condition, and implemented adequate
*  
      compensatory measures for out-of-service, degraded, or inoperable fire protection
fire zone 318 - cable spreading room;  
      equipment, systems, or features in accordance with the licensee's fire plan.
*  
      The inspectors selected fire areas based on their overall contribution to internal fire risk
fire zone 775 - G-04 emergency diesel generator (EDG); and  
      and their potential to impact equipment that could initiate or mitigate a plant transient.
*  
      The inspectors verified that fire hoses and extinguishers were in their designated
fire zone 301 - Unit 2 turbine building basement.  
      locations and available for immediate use; fire detectors and sprinklers were
The inspectors reviewed areas to assess if the licensee had implemented a fire  
      unobstructed; transient material loading was within the analyzed limits; and fire doors,
protection program that adequately controlled combustibles and ignition sources within  
      dampers, and penetration seals appeared to be in satisfactory condition. The inspectors
the plant, effectively maintained fire detection and suppression capability, maintained  
      also verified that minor issues identified during the inspection were entered into the
passive fire protection features in good material condition, and implemented adequate  
      licensee's CAP. Documents reviewed are listed in the Attachment to this report.
compensatory measures for out-of-service, degraded, or inoperable fire protection  
      These activities constituted four quarterly fire protection inspection samples as defined in
equipment, systems, or features in accordance with the licensee's fire plan.
      IP 71111.05-05.
The inspectors selected fire areas based on their overall contribution to internal fire risk  
  b. Findings
and their potential to impact equipment that could initiate or mitigate a plant transient.
      No findings of significance were identified.
The inspectors verified that fire hoses and extinguishers were in their designated  
.2   Annual Fire Protection Drill Observation (71111.05A)
locations and available for immediate use; fire detectors and sprinklers were  
  a. Inspection Scope
unobstructed; transient material loading was within the analyzed limits; and fire doors,  
      On December 10, 2009, the inspectors observed a fire brigade activation in the north
dampers, and penetration seals appeared to be in satisfactory condition. The inspectors  
      service building in response to a simulated electrical fire in the warehouse storeroom.
also verified that minor issues identified during the inspection were entered into the  
      Based on this observation, the inspectors completed an annual evaluation of the
licensee's CAP. Documents reviewed are listed in the Attachment to this report.  
      readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee
These activities constituted four quarterly fire protection inspection samples as defined in  
      staff identified deficiencies, openly discussed them in a self-critical manner at the drill
IP 71111.05-05.  
      debrief, and took appropriate corrective actions. Specific attributes evaluated were:
b.  
      (1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper
Findings  
      use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;
No findings of significance were identified.  
      (4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade
.2  
      leader communications, command, and control; (6) search for victims and propagation of
Annual Fire Protection Drill Observation (71111.05A)  
                                                  7                                      Enclosure
a.  
Inspection Scope  
On December 10, 2009, the inspectors observed a fire brigade activation in the north  
service building in response to a simulated electrical fire in the warehouse storeroom.
Based on this observation, the inspectors completed an annual evaluation of the  
readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee  
staff identified deficiencies, openly discussed them in a self-critical manner at the drill  
debrief, and took appropriate corrective actions. Specific attributes evaluated were:
(1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper  
use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;  
(4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade  
leader communications, command, and control; (6) search for victims and propagation of  


      the fire into other plant areas; (7) smoke removal operations; (8) utilization of
      pre-planned strategies; (9) adherence to the pre-planned drill scenario; and
Enclosure
      (10) drill objectives. Documents reviewed are listed in the Attachment to this report.
8
      These activities constituted one annual fire protection inspection sample as defined in
the fire into other plant areas; (7) smoke removal operations; (8) utilization of  
      IP 71111.05-05.
pre-planned strategies; (9) adherence to the pre-planned drill scenario; and  
  b. Findings
(10) drill objectives. Documents reviewed are listed in the Attachment to this report.  
      No findings of significance were identified.
These activities constituted one annual fire protection inspection sample as defined in  
1R06 Flooding (71111.06)
IP 71111.05-05.  
.1   Internal Flooding
b.  
  a. Inspection Scope
Findings  
      The inspectors reviewed selected important-to-safety plant design features and licensee
No findings of significance were identified.  
      procedures intended to protect the plant and its safety-related equipment from internal
1R06 Flooding (71111.06)  
      flooding events. The inspectors reviewed flood analyses and design documents,
.1  
      including the FSAR, engineering calculations, and abnormal operating procedures to
Internal Flooding  
      identify licensee commitments. In addition, the inspectors reviewed licensee drawings to
a.  
      identify areas and equipment that may be affected by internal flooding caused by the
Inspection Scope  
      failure or misalignment of nearby sources of water, such as the fire suppression or the
The inspectors reviewed selected important-to-safety plant design features and licensee  
      circulating water systems. The inspectors also reviewed the licensee's corrective action
procedures intended to protect the plant and its safety-related equipment from internal  
      documents with respect to past flood-related items identified in the CAP to verify the
flooding events. The inspectors reviewed flood analyses and design documents,  
      adequacy of the corrective actions. The inspectors performed a walkdown of the
including the FSAR, engineering calculations, and abnormal operating procedures to  
      following plant area to assess the adequacy of flood protection and mitigation features,
identify licensee commitments. In addition, the inspectors reviewed licensee drawings to  
      verify drains and sumps were clear of debris and were functional, and verify that the
identify areas and equipment that may be affected by internal flooding caused by the  
      licensee complied with its commitments. Documents reviewed are listed in the
failure or misalignment of nearby sources of water, such as the fire suppression or the  
      Attachment to this report.
circulating water systems. The inspectors also reviewed the licensee's corrective action  
      *       G-01 and G-02 EDG rooms.
documents with respect to past flood-related items identified in the CAP to verify the  
      This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
adequacy of the corrective actions. The inspectors performed a walkdown of the  
  b. Findings
following plant area to assess the adequacy of flood protection and mitigation features,  
      No findings of significance were identified.
verify drains and sumps were clear of debris and were functional, and verify that the  
1R08 Inservice Inspection (ISI) Activities (71111.08P)
licensee complied with its commitments. Documents reviewed are listed in the  
      From November 2 through November 6, 2009, the inspectors conducted a review of the
Attachment to this report.  
      implementation of the licensee's ISI program for monitoring degradation of the reactor
*  
      coolant system (RCS), steam generator (SG) tubes, AFW systems, risk-significant piping
G-01 and G-02 EDG rooms.  
      and components, and containment systems.
This inspection constituted one internal flooding sample as defined in IP 71111.06-05.  
      The inspections described in Sections 1R08.1, 1R08.2, 1R08.3, 1R08.4, and 1R08.5
b.  
      below constituted one ISI sample as defined in IP 71111.08-05.
Findings  
                                                8                                      Enclosure
No findings of significance were identified.  
1R08 Inservice Inspection (ISI) Activities (71111.08P)  
From November 2 through November 6, 2009, the inspectors conducted a review of the  
implementation of the licensee's ISI program for monitoring degradation of the reactor  
coolant system (RCS), steam generator (SG) tubes, AFW systems, risk-significant piping  
and components, and containment systems.  
The inspections described in Sections 1R08.1, 1R08.2, 1R08.3, 1R08.4, and 1R08.5  
below constituted one ISI sample as defined in IP 71111.08-05.  


.1   Piping Systems ISI
  a. Inspection Scope
Enclosure
      The inspectors observed and reviewed records of the following nondestructive
9
      examinations mandated by the American Society of Mechanical Engineers (ASME)
.1  
      Section XI Code to evaluate compliance with the ASME Code Section XI and Section V
Piping Systems ISI  
      requirements and if any indications and defects detected were detected, and to
a. Inspection Scope  
      determine if these were dispositioned in accordance with the ASME Code or an
The inspectors observed and reviewed records of the following nondestructive  
      NRC-approved alternative requirement.
examinations mandated by the American Society of Mechanical Engineers (ASME)  
      *       ultrasonic examination of steam generator shell-to-head circumferential weld
Section XI Code to evaluate compliance with the ASME Code Section XI and Section V  
              SG-A-5R1 (Report No. 2009UT-22);
requirements and if any indications and defects detected were detected, and to  
      *       liquid penetrant examination of reactor closure head peripheral control rod drive
determine if these were dispositioned in accordance with the ASME Code or an  
              mechanism housings 28 and 32 welds (Report No. 2009PT-001); and
NRC-approved alternative requirement.  
      *       ultrasonic examination of the reactor coolant system pressurizer surge nozzle
*  
              inside radius section weld (Report No. 2009UT-057).
ultrasonic examination of steam generator shell-to-head circumferential weld  
      The inspectors reviewed records of the following nondestructive examinations conducted
SG-A-5R1 (Report No. 2009UT-22);  
      as part of the licensee's industry initiative inspection program for primary water stress
*  
      corrosion cracking to determine if the examinations were conducted in accordance with
liquid penetrant examination of reactor closure head peripheral control rod drive  
      the licensee's augmented inspection program, industry guidance documents, and
mechanism housings 28 and 32 welds (Report No. 2009PT-001); and  
      associated licensee examination procedures, and if any indications and defects were
*  
      detected, to determine if these were dispositioned in accordance with approved
ultrasonic examination of the reactor coolant system pressurizer surge nozzle  
      procedures and NRC requirements.
inside radius section weld (Report No. 2009UT-057).  
      *       visual examination of SG outlet nozzle-to-safe end weld RC-36-MRCL-AII-01A
The inspectors reviewed records of the following nondestructive examinations conducted  
              (Report No. 2009VT-031);
as part of the licensee's industry initiative inspection program for primary water stress  
      *       visual examination of SG safe-end to "A" S/G inlet nozzle weld
corrosion cracking to determine if the examinations were conducted in accordance with  
              RC-34-MRCL-AI-05 (Report No. 2009VT-030);
the licensee's augmented inspection program, industry guidance documents, and  
      *       visual examination of SG "A" cold leg vent nozzle, (Report No. 2009VT-029); and
associated licensee examination procedures, and if any indications and defects were  
      *       visual examination of SG "A" hot leg vent nozzle, (Report No. 2009VT-028).
detected, to determine if these were dispositioned in accordance with approved  
      There were no examinations completed during the previous outage with relevant or
procedures and NRC requirements.  
      recordable conditions or indications accepted for continued service. Therefore, no
*  
      NRC review was completed for this inspection procedure attribute.
visual examination of SG outlet nozzle-to-safe end weld RC-36-MRCL-AII-01A  
      The inspectors reviewed the following pressure boundary weld repairs completed on
(Report No. 2009VT-031);  
      risk-significant systems since the beginning of the last refueling outage (RFO) to verify
*  
      that the welding and any associated non-destructive examinations were performed in
visual examination of SG safe-end to "A" S/G inlet nozzle weld  
      accordance with the Construction Code and ASME Code, Section XI. Additionally, the
RC-34-MRCL-AI-05 (Report No. 2009VT-030);  
      inspectors reviewed the welding procedure specification and supporting weld procedure
*  
      qualification records to determine if the weld procedure(s) were qualified in accordance
visual examination of SG "A" cold leg vent nozzle, (Report No. 2009VT-029); and  
      with the requirements of Construction Code and the ASME Section IX Code.
*  
      *       Work Order 00352831, Replacement of an ASME Section III, Class 1,
visual examination of SG "A" hot leg vent nozzle, (Report No. 2009VT-028).  
              Excess Letdown Heat Exchanger (ELHX) 2HX-4 Outlet Drain Valve 2CV-D-11;
There were no examinations completed during the previous outage with relevant or  
              and
recordable conditions or indications accepted for continued service. Therefore, no  
      *       Work Order 00352519, Replacement of an ASME Section III, Class 1, RCS to
NRC review was completed for this inspection procedure attribute.  
              P-10A/B Residual Heat Removal (RHR) Pump Suction Header Drain
The inspectors reviewed the following pressure boundary weld repairs completed on  
              Valve 2RH-D-9.
risk-significant systems since the beginning of the last refueling outage (RFO) to verify  
                                                  9                                    Enclosure
that the welding and any associated non-destructive examinations were performed in  
accordance with the Construction Code and ASME Code, Section XI. Additionally, the  
inspectors reviewed the welding procedure specification and supporting weld procedure  
qualification records to determine if the weld procedure(s) were qualified in accordance  
with the requirements of Construction Code and the ASME Section IX Code.  
*  
Work Order 00352831, Replacement of an ASME Section III, Class 1,  
Excess Letdown Heat Exchanger (ELHX) 2HX-4 Outlet Drain Valve 2CV-D-11;  
and  
*  
Work Order 00352519, Replacement of an ASME Section III, Class 1, RCS to  
P-10A/B Residual Heat Removal (RHR) Pump Suction Header Drain  
Valve 2RH-D-9.  


  b. Findings
      No findings of significance were identified.
Enclosure
.2   Reactor Pressure Vessel Upper Head Penetration Inspection Activities
10
  a. Inspection Scope
b. Findings  
      For the Unit 2 reactor vessel head, a bare metal visual examination was required this
No findings of significance were identified.  
      outage pursuant to 10 CFR 50.55a(g)(6)(ii)(D).
.2  
      The inspectors reviewed records of the visual examination conducted on the Unit 2
Reactor Pressure Vessel Upper Head Penetration Inspection Activities  
      reactor vessel head at penetrations 16, 32, and 40 to determine if the activities were
a.  
      conducted in accordance with the requirements of ASME Code Case N-729-1 and
Inspection Scope  
      10 CFR 50.55a(g)(6)(ii)(D). In particular, the inspectors confirmed that:
For the Unit 2 reactor vessel head, a bare metal visual examination was required this  
      *       the required visual examination scope/coverage was achieved in accordance
outage pursuant to 10 CFR 50.55a(g)(6)(ii)(D).  
              with the licensee's procedures; and
The inspectors reviewed records of the visual examination conducted on the Unit 2  
      *       the criteria for visual examination quality and instructions for resolving
reactor vessel head at penetrations 16, 32, and 40 to determine if the activities were  
              interference and masking issues were adequate.
conducted in accordance with the requirements of ASME Code Case N-729-1 and  
      No indications of potential through-wall leakage were identified by the licensee.
10 CFR 50.55a(g)(6)(ii)(D). In particular, the inspectors confirmed that:  
      Therefore, no NRC review was completed for this IP attribute.
*  
      The licensee did not perform any welded repairs to vessel head penetrations since the
the required visual examination scope/coverage was achieved in accordance  
      beginning of the preceding outage for Unit 2. Therefore, no NRC review was completed
with the licensee's procedures; and  
      for this IP attribute.
*  
  b. Findings
the criteria for visual examination quality and instructions for resolving  
      No findings of significance were identified.
interference and masking issues were adequate.  
.3   Boric Acid Corrosion Control (BACC)
No indications of potential through-wall leakage were identified by the licensee.
  a. Inspection Scope
Therefore, no NRC review was completed for this IP attribute.  
      The inspectors observed and reviewed records of the licensee's initial BACC visual
The licensee did not perform any welded repairs to vessel head penetrations since the  
      examinations and verified whether these visual examinations emphasized locations
beginning of the preceding outage for Unit 2. Therefore, no NRC review was completed  
      where boric acid leaks could cause degradation of safety-significant components.
for this IP attribute.  
      The inspectors reviewed the following licensee evaluations of RCS components with
b.  
      boric acid deposits to determine if degraded components were documented in the CAP.
Findings  
      The inspectors also evaluated corrective actions for any degraded RCS components to
No findings of significance were identified.  
      determine if they met the component Construction Code, ASME Section XI Code, and/or
.3  
      NRC-approved alternative.
Boric Acid Corrosion Control (BACC)  
      *       boric acid evaluation No. 09-219, 2SC-953 boric acid indications; and
a. Inspection Scope  
      *       boric acid evaluation No. 09-173B, 2P-116, 2T-6C BA tank recirculation pump.
The inspectors observed and reviewed records of the licensee's initial BACC visual  
      The inspectors reviewed the following corrective actions related to evidence of boric acid
examinations and verified whether these visual examinations emphasized locations  
      leakage to determine if the corrective actions completed were consistent with the
where boric acid leaks could cause degradation of safety-significant components.  
                                                10                                      Enclosure
The inspectors reviewed the following licensee evaluations of RCS components with  
boric acid deposits to determine if degraded components were documented in the CAP.
The inspectors also evaluated corrective actions for any degraded RCS components to  
determine if they met the component Construction Code, ASME Section XI Code, and/or  
NRC-approved alternative.  
*  
boric acid evaluation No. 09-219, 2SC-953 boric acid indications; and  
*  
boric acid evaluation No. 09-173B, 2P-116, 2T-6C BA tank recirculation pump.  
The inspectors reviewed the following corrective actions related to evidence of boric acid  
leakage to determine if the corrective actions completed were consistent with the  


      requirements of the ASME Section XI Code and 10 CFR Part 50, Appendix B,
      Criterion XVI.
Enclosure
      *       Work Order Package 0035658301, Replace Pump Mechanical Seal; and
11
      *       Work Request No. 00039792, Adjust Packing to Last Value During AOV
requirements of the ASME Section XI Code and 10 CFR Part 50, Appendix B,  
                [air operated valve] Diagnostics.
Criterion XVI.  
    b. Findings
*  
      No findings of significance were identified.
Work Order Package 0035658301, Replace Pump Mechanical Seal; and  
.4   Steam Generator Tube Inspection Activities
*  
    a. Inspection Scope
Work Request No. 00039792, Adjust Packing to Last Value During AOV  
      For the Unit 2 SGs, no examination was required pursuant to the TSs during the current
[air operated valve] Diagnostics.  
      RFO, U2R30. Therefore, no NRC review was completed for this IP attribute.
b. Findings  
    b. Findings
No findings of significance were identified.  
      No findings of significance were identified.
.4  
.5   Identification and Resolution of Problems
Steam Generator Tube Inspection Activities  
    a. Inspection Scope
a. Inspection Scope  
      The inspectors performed a review of ISI/SG-related problems entered into the
For the Unit 2 SGs, no examination was required pursuant to the TSs during the current  
      licensee's CAP and conducted interviews with licensee staff to determine if:
RFO, U2R30. Therefore, no NRC review was completed for this IP attribute.  
      *       the licensee had established an appropriate threshold for identifying
b. Findings  
                ISI/SG-related problems;
No findings of significance were identified.  
      *       the licensee had taken appropriate corrective actions; and
.5  
      *       the licensee had evaluated operating experience and industry generic issues
Identification and Resolution of Problems  
                related to ISI and pressure boundary integrity.
a. Inspection Scope  
      The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,
The inspectors performed a review of ISI/SG-related problems entered into the  
      Appendix B, Criterion XVI, "Corrective Action," requirements. The corrective action
licensee's CAP and conducted interviews with licensee staff to determine if:  
      documents reviewed by the inspectors are listed in the Attachment to this report.
*  
  b.   Findings
the licensee had established an appropriate threshold for identifying  
      No findings of significance were identified.
ISI/SG-related problems;  
1R11 Licensed Operator Requalification Program (71111.11)
*  
.1   Resident Inspector Quarterly Review (71111.11Q)
the licensee had taken appropriate corrective actions; and  
  a. Inspection Scope
*  
      On December 1, 2009, the inspectors observed a crew of licensed operators in the
the licensee had evaluated operating experience and industry generic issues  
      plant's simulator during just-in-time training for the Unit 2 startup to verify that operator
related to ISI and pressure boundary integrity.  
                                                  11                                        Enclosure
The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,  
Appendix B, Criterion XVI, "Corrective Action," requirements. The corrective action  
documents reviewed by the inspectors are listed in the Attachment to this report.  
b.  
Findings  
No findings of significance were identified.  
1R11 Licensed Operator Requalification Program (71111.11)  
.1  
Resident Inspector Quarterly Review (71111.11Q)  
a.  
Inspection Scope  
On December 1, 2009, the inspectors observed a crew of licensed operators in the  
plant's simulator during just-in-time training for the Unit 2 startup to verify that operator  


    performance was adequate, evaluators were identifying and documenting crew
    performance problems, and training was being conducted in accordance with licensee
Enclosure
    procedures. The inspectors evaluated the following areas:
12
    *       licensed operator performance;
performance was adequate, evaluators were identifying and documenting crew  
    *       crew's clarity and formality of communications;
performance problems, and training was being conducted in accordance with licensee  
    *       ability to take timely actions in the conservative direction;
procedures. The inspectors evaluated the following areas:  
    *       prioritization, interpretation, and verification of annunciator alarms;
*  
    *       correct use and implementation of abnormal and emergency procedures;
licensed operator performance;  
    *       control board manipulations;
*  
    *       oversight and direction from supervisors; and
crew's clarity and formality of communications;  
    *       ability to identify and implement appropriate TS actions and Emergency Plan
*  
              actions and notifications.
ability to take timely actions in the conservative direction;  
    The crew's performance in these areas was compared to pre-established operator action
*  
    expectations and successful critical task completion requirements. Documents reviewed
prioritization, interpretation, and verification of annunciator alarms;  
    are listed in the Attachment to this report.
*  
    This inspection constituted one quarterly licensed operator requalification program
correct use and implementation of abnormal and emergency procedures;  
    sample as defined in IP 71111.11.
*  
  b. Findings
control board manipulations;  
    No findings of significance were identified.
*  
.2   Annual Operating Test Results (71111.11B)
oversight and direction from supervisors; and  
  a. Inspection Scope
*  
    The inspectors reviewed the overall pass/fail results of the individual Job Performance
ability to identify and implement appropriate TS actions and Emergency Plan  
    Measure operating tests, and the simulator operating tests (required to be given
actions and notifications.  
    per 10 CFR 55.59(a)(2)) administered by the licensee from August 10 through
The crew's performance in these areas was compared to pre-established operator action  
    October 1, 2009, as part of the licensee's operator licensing requalification cycle.
expectations and successful critical task completion requirements. Documents reviewed  
    These results were compared to the thresholds established in IMC 0609, Appendix I,
are listed in the Attachment to this report.  
    "Licensed Operator Requalification Significance Determination Process."
This inspection constituted one quarterly licensed operator requalification program  
    The evaluations were also performed to determine if the licensee effectively
sample as defined in IP 71111.11.  
    implemented operator requalification guidelines established in NUREG 1021,
b.  
    "Operator Licensing Examination Standards for Power Reactors," and IP 71111.11,
Findings  
    "Licensed Operator Requalification Program." Documents reviewed are listed in the
No findings of significance were identified.  
    Attachment to this report.
.2  
    Completion of this section constituted one biennial licensed operator requalification
Annual Operating Test Results (71111.11B)  
    inspection sample as defined in IP 71111.11B.
a.  
  b. Findings
Inspection Scope  
    No findings of significance were identified.
The inspectors reviewed the overall pass/fail results of the individual Job Performance  
                                                  12                                  Enclosure
Measure operating tests, and the simulator operating tests (required to be given  
per 10 CFR 55.59(a)(2)) administered by the licensee from August 10 through  
October 1, 2009, as part of the licensee's operator licensing requalification cycle.
These results were compared to the thresholds established in IMC 0609, Appendix I,  
"Licensed Operator Requalification Significance Determination Process."
The evaluations were also performed to determine if the licensee effectively  
implemented operator requalification guidelines established in NUREG 1021,  
"Operator Licensing Examination Standards for Power Reactors," and IP 71111.11,  
"Licensed Operator Requalification Program." Documents reviewed are listed in the  
Attachment to this report.  
Completion of this section constituted one biennial licensed operator requalification  
inspection sample as defined in IP 71111.11B.  
b.  
Findings  
No findings of significance were identified.  


1R12 Maintenance Effectiveness (71111.12)
.1   Containment Accident Fan Cooler Units (71111.12Q)
Enclosure
  a. Inspection Scope
13
      The inspectors evaluated degraded performance issues involving the following
1R12 Maintenance Effectiveness (71111.12)  
      risk-significant system:
.1  
      *       containment accident fan cooler units.
Containment Accident Fan Cooler Units (71111.12Q)  
      The inspectors reviewed events, such as where ineffective equipment maintenance had
a.  
      resulted in valid or invalid automatic actuations of engineered safeguards systems, and
Inspection Scope  
      independently verified the licensee's actions to address system performance or condition
The inspectors evaluated degraded performance issues involving the following  
      problems in terms of the following:
risk-significant system:  
      *       implementing appropriate work practices;
*  
      *       identifying and addressing common cause failures;
containment accident fan cooler units.  
      *       scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
The inspectors reviewed events, such as where ineffective equipment maintenance had  
      *       characterizing system reliability issues for performance;
resulted in valid or invalid automatic actuations of engineered safeguards systems, and  
      *       charging unavailability for performance;
independently verified the licensee's actions to address system performance or condition  
      *       trending key parameters for condition monitoring;
problems in terms of the following:  
      *       ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
*  
      *       verifying appropriate performance criteria for structures, systems, and
implementing appropriate work practices;  
              components/functions classified as (a)(2) or appropriate and adequate goals and
*  
              corrective actions for systems classified as (a)(1).
identifying and addressing common cause failures;  
      The inspectors assessed performance issues with respect to the reliability, availability,
*  
      and condition monitoring of the system. In addition, the inspectors verified maintenance
scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
      effectiveness issues were entered into the CAP with the appropriate significance
*  
      characterization. Documents reviewed are listed in the Attachment to this report.
characterizing system reliability issues for performance;  
      This inspection constituted one quarterly maintenance effectiveness sample as defined
*  
      in IP 71111.12-05.
charging unavailability for performance;  
  b. Findings
*  
      Failure to Meet Generic Letter (GL) 89-13 Program for Mussel Control
trending key parameters for condition monitoring;  
      Introduction: The inspectors identified a Green finding for the failure to meet a
*  
      GL 89-13, "Service Water System Problems Affecting Safety-Related Equipment,"
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and  
      program commitment. Specifically, the licensee committed to implement mussel control
*  
      methods to prevent fouling of safety-related heat exchangers. The 2008 annual biocide
verifying appropriate performance criteria for structures, systems, and  
      treatment for mussel control was not conducted and excessive tube blockage and
components/functions classified as (a)(2) or appropriate and adequate goals and  
      reduced flow to safety-related heat exchangers due to mussels was identified after
corrective actions for systems classified as (a)(1).  
      treatment in 2009.
The inspectors assessed performance issues with respect to the reliability, availability,  
      Description: In response to GL 89-13, Point Beach developed a program documenting
and condition monitoring of the system. In addition, the inspectors verified maintenance  
      GL 89-13 commitments made to the NRC. Among those commitments was one to
effectiveness issues were entered into the CAP with the appropriate significance  
      implement a biofouling program for mussel control and eradication to prevent fouling of
characterization. Documents reviewed are listed in the Attachment to this report.  
      safety-related components.
This inspection constituted one quarterly maintenance effectiveness sample as defined  
                                                13                                      Enclosure
in IP 71111.12-05.  
b.  
Findings  
Failure to Meet Generic Letter (GL) 89-13 Program for Mussel Control  
Introduction: The inspectors identified a Green finding for the failure to meet a  
GL 89-13, "Service Water System Problems Affecting Safety-Related Equipment,"  
program commitment. Specifically, the licensee committed to implement mussel control  
methods to prevent fouling of safety-related heat exchangers. The 2008 annual biocide  
treatment for mussel control was not conducted and excessive tube blockage and  
reduced flow to safety-related heat exchangers due to mussels was identified after  
treatment in 2009.  
Description: In response to GL 89-13, Point Beach developed a program documenting  
GL 89-13 commitments made to the NRC. Among those commitments was one to  
implement a biofouling program for mussel control and eradication to prevent fouling of  
safety-related components.  


In 1999, the plant experienced significant mussel blockage events after not performing a
biocide treatment in the previous year. In 2000, a licensee review of the mussel control
Enclosure
strategy determined that two biocide treatments per year should be implemented so that
14
mussels did not grow to a size that would block heat exchanger tubes when the shells
In 1999, the plant experienced significant mussel blockage events after not performing a  
detach from the piping. However, since that time, the plant performed only one biocide
biocide treatment in the previous year. In 2000, a licensee review of the mussel control  
treatment per year, which empirically appeared adequate.
strategy determined that two biocide treatments per year should be implemented so that  
In August 2008, the annual mussel biocide treatment was deferred due to concerns by
mussels did not grow to a size that would block heat exchanger tubes when the shells  
operations that the treatment would impact the operation of safety-related components.
detach from the piping. However, since that time, the plant performed only one biocide  
The decision, however, was made without consulting the GL 89-13 program engineer or
treatment per year, which empirically appeared adequate.  
the service water (SW) system engineer. It was possible to defer the treatment with
In August 2008, the annual mussel biocide treatment was deferred due to concerns by  
minimal reviews since the WO was inappropriately categorized as a low Priority 4,
operations that the treatment would impact the operation of safety-related components.
"other," task.
The decision, however, was made without consulting the GL 89-13 program engineer or  
The missed biocide treatment was documented in the CAP as Action Request (AR)
the service water (SW) system engineer. It was possible to defer the treatment with  
1133110, and corrective actions were implemented. None of the corrective actions
minimal reviews since the WO was inappropriately categorized as a low Priority 4,  
discussed rescheduling the biocide treatment in 2008. Instead, the decision was made
"other," task.  
to perform the SW system biocide treatments for Unit 1 in spring and fall 2009, and for
The missed biocide treatment was documented in the CAP as Action Request (AR)  
Unit 2 in fall 2009, just prior to the RFO. This schedule resulted in the Unit 2 SW system
1133110, and corrective actions were implemented. None of the corrective actions  
not being treated for about two years.
discussed rescheduling the biocide treatment in 2008. Instead, the decision was made  
The Unit 2 mussel biocide treatment was completed on October 8, 2009. The following
to perform the SW system biocide treatments for Unit 1 in spring and fall 2009, and for  
day, Unit 2 entered an unexpected Technical Specification Action Condition (TSAC) due
Unit 2 in fall 2009, just prior to the RFO. This schedule resulted in the Unit 2 SW system  
to low flow in containment fan cooler (CFC) 2HX-15D. Flow was promptly increased by
not being treated for about two years.  
operations, and the TSAC was exited. Subsequently, during the Unit 2 outage (within a
The Unit 2 mussel biocide treatment was completed on October 8, 2009. The following  
month of the biocide treatment) the component cooling water heat exchangers
day, Unit 2 entered an unexpected Technical Specification Action Condition (TSAC) due  
(CCWHXs), 2HX-12D and 0HX-12C (those affected by the Unit 2 biocide treatment), and
to low flow in containment fan cooler (CFC) 2HX-15D. Flow was promptly increased by  
the Unit 2 CFCs, 2HX-15A, 2HX-15C, and 2HX-15D, were opened for inspection.
operations, and the TSAC was exited. Subsequently, during the Unit 2 outage (within a  
The CCWHXs acceptance criterion for the number of tubes blocked was 160 tubes.
month of the biocide treatment) the component cooling water heat exchangers  
In 2HX-12D, 828 tubes were found blocked and in 0HX-12C, 507 tubes were blocked by
(CCWHXs), 2HX-12D and 0HX-12C (those affected by the Unit 2 biocide treatment), and  
mussel shells. The CFCs acceptance criterion for blocked tubes is 25 tubes. The plant
the Unit 2 CFCs, 2HX-15A, 2HX-15C, and 2HX-15D, were opened for inspection.
identified 46, 107, and 77 tubes blocked by mussel shells in 2HX-15A, 2HX-15C, and
The CCWHXs acceptance criterion for the number of tubes blocked was 160 tubes.
2HX-15D respectively. The 2HX-15B CFC was found acceptable. All heat exchangers
In 2HX-12D, 828 tubes were found blocked and in 0HX-12C, 507 tubes were blocked by  
were cleaned and mussel shells removed from the tubes. The inspectors reviewed the
mussel shells. The CFCs acceptance criterion for blocked tubes is 25 tubes. The plant  
licensees evaluation of past operability for the unacceptable CCWHXs, which concluded
identified 46, 107, and 77 tubes blocked by mussel shells in 2HX-15A, 2HX-15C, and  
they had been operable during power operations, and found no issues.
2HX-15D respectively. The 2HX-15B CFC was found acceptable. All heat exchangers  
Analysis: The inspectors determined that the failure to prevent fouling of safety-related
were cleaned and mussel shells removed from the tubes. The inspectors reviewed the  
heat exchangers in accordance with GL 89-13 commitments was a performance
licensees evaluation of past operability for the unacceptable CCWHXs, which concluded  
deficiency. Specifically, the deferral of the 2008 biocide treatment allowed mussels to
they had been operable during power operations, and found no issues.  
grow to sufficient size that they would no longer pass through the heat exchanger tubes
Analysis: The inspectors determined that the failure to prevent fouling of safety-related  
and the licensee could have reasonably been expected to prevent this based on past
heat exchangers in accordance with GL 89-13 commitments was a performance  
experience. The finding was determined to be more than minor because the finding was
deficiency. Specifically, the deferral of the 2008 biocide treatment allowed mussels to  
associated with the Mitigating Systems Cornerstone attribute of equipment performance
grow to sufficient size that they would no longer pass through the heat exchanger tubes  
and adversely affected the associated cornerstone objective of ensuring the reliability
and the licensee could have reasonably been expected to prevent this based on past  
and capability of systems that respond to initiating events to prevent undesirable
experience. The finding was determined to be more than minor because the finding was  
consequences. Specifically, the failure to perform the 2008 biocide treatment affected
associated with the Mitigating Systems Cornerstone attribute of equipment performance  
the operability and design requirements of the CCWHXs and the CFCs.
and adversely affected the associated cornerstone objective of ensuring the reliability  
The inspectors determined the finding could be evaluated using the SDP in accordance
and capability of systems that respond to initiating events to prevent undesirable  
with IMC 0609, "Significance Determination Process," Attachment 0609.04,
consequences. Specifically, the failure to perform the 2008 biocide treatment affected  
                                          14                                    Enclosure
the operability and design requirements of the CCWHXs and the CFCs.  
The inspectors determined the finding could be evaluated using the SDP in accordance  
with IMC 0609, "Significance Determination Process," Attachment 0609.04,  


    "Phase 1 - Initial Screening and Characterization of Findings," Table 4a, for the
    Mitigating Systems Cornerstone, dated January 10, 2008. The finding was determined
Enclosure
    to be of very low safety significance (Green) because the issue did not result in the
15
    actual loss of a safety function or loss of a single train for greater than its allowed
"Phase 1 - Initial Screening and Characterization of Findings," Table 4a, for the  
    TS time, and did not screen as potentially risk-significant due to seismic, flooding, or
Mitigating Systems Cornerstone, dated January 10, 2008. The finding was determined  
    severe weather initiating events. The inspectors determined this performance deficiency
to be of very low safety significance (Green) because the issue did not result in the  
    was not indicative of current performance and therefore no cross-cutting issue was
actual loss of a safety function or loss of a single train for greater than its allowed  
    identified.
TS time, and did not screen as potentially risk-significant due to seismic, flooding, or  
    Enforcement: No violation of regulatory requirements occurred because this issue
severe weather initiating events. The inspectors determined this performance deficiency  
    represents a failure to implement an NRC commitment. This finding was entered into
was not indicative of current performance and therefore no cross-cutting issue was  
    the licensee's CAP as AR 01158115 (FIN 05000266/2009005-01;
identified.  
    05000301/2009005-01).
Enforcement: No violation of regulatory requirements occurred because this issue  
    In response to this issue, the licensee adjusted flow through the affected heat
represents a failure to implement an NRC commitment. This finding was entered into  
    exchangers to address the immediate low flow conditions in addition to opening and
the licensee's CAP as AR 01158115 (FIN 05000266/2009005-01;  
    cleaning all affected heat exchangers to remove mussel shells. In addition, the licensee
05000301/2009005-01).  
    raised the priority of future annual biocide treatments by designating them as preventive
In response to this issue, the licensee adjusted flow through the affected heat  
    maintenance tasks. This re-designation will require more extensive reviews and
exchangers to address the immediate low flow conditions in addition to opening and  
    approvals if a plan to defer an annual treatment arises.
cleaning all affected heat exchangers to remove mussel shells. In addition, the licensee  
.2   Routine Quarterly Evaluations (71111.12Q)
raised the priority of future annual biocide treatments by designating them as preventive  
  a. Inspection Scope
maintenance tasks. This re-designation will require more extensive reviews and  
    The inspectors evaluated degraded performance issues involving the following
approvals if a plan to defer an annual treatment arises.  
    risk-significant system:
.2  
    *       gas turbine system.
Routine Quarterly Evaluations (71111.12Q)  
    The inspectors reviewed events such as where ineffective equipment maintenance had
a.  
    resulted in valid or invalid automatic actuations of engineered safeguards systems and
Inspection Scope  
    independently verified the licensee's actions to address system performance or condition
The inspectors evaluated degraded performance issues involving the following  
    problems in terms of the following:
risk-significant system:  
    *       implementing appropriate work practices;
*  
    *       identifying and addressing common cause failures;
gas turbine system.  
    *       scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
The inspectors reviewed events such as where ineffective equipment maintenance had  
    *       characterizing system reliability issues for performance;
resulted in valid or invalid automatic actuations of engineered safeguards systems and  
    *       charging unavailability for performance;
independently verified the licensee's actions to address system performance or condition  
    *       trending key parameters for condition monitoring;
problems in terms of the following:  
    *       ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
*  
    *       verifying appropriate performance criteria for structures, systems, and
implementing appropriate work practices;  
              components/functions classified as (a)(2) or appropriate and adequate goals and
*  
              corrective actions for systems classified as (a)(1).
identifying and addressing common cause failures;  
    The inspectors assessed performance issues with respect to the reliability, availability,
*  
    and condition monitoring of the system. In addition, the inspectors verified maintenance
scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
    effectiveness issues were entered into the CAP with the appropriate significance
*  
    characterization. Documents reviewed are listed in the Attachment to this report.
characterizing system reliability issues for performance;  
                                                15                                        Enclosure
*  
charging unavailability for performance;  
*  
trending key parameters for condition monitoring;  
*  
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and  
*  
verifying appropriate performance criteria for structures, systems, and  
components/functions classified as (a)(2) or appropriate and adequate goals and  
corrective actions for systems classified as (a)(1).  
The inspectors assessed performance issues with respect to the reliability, availability,  
and condition monitoring of the system. In addition, the inspectors verified maintenance  
effectiveness issues were entered into the CAP with the appropriate significance  
characterization. Documents reviewed are listed in the Attachment to this report.  


      This inspection constituted one quarterly maintenance effectiveness sample as defined
      in IP 71111.12-05.
Enclosure
  b. Findings
16
      No findings of significance were identified.
This inspection constituted one quarterly maintenance effectiveness sample as defined  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
in IP 71111.12-05.  
.1   Maintenance Risk Assessments and Emergent Work Control
b.  
  a. Inspection Scope
Findings  
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
No findings of significance were identified.  
      maintenance and emergent work activities affecting risk-significant and safety-related
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
      equipment listed below to verify that the appropriate risk assessments were performed
.1  
      prior to removing equipment for work:
Maintenance Risk Assessments and Emergent Work Control  
      *       week of November 16, 2009, following the circulating water grass intrusion event
a.  
              and inverter trouble.
Inspection Scope  
      These activities were selected based on their potential risk significance relative to the
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
      Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
maintenance and emergent work activities affecting risk-significant and safety-related  
      risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
equipment listed below to verify that the appropriate risk assessments were performed  
      and complete. When emergent work was performed, the inspectors verified that the
prior to removing equipment for work:  
      plant risk was promptly reassessed and managed. The inspectors reviewed the scope
*  
      of maintenance work, discussed the results of the assessment with the licensee's
week of November 16, 2009, following the circulating water grass intrusion event  
      probabilistic risk analyst or shift technical advisor, and verified plant conditions were
and inverter trouble.  
      consistent with the risk assessment. The inspectors also reviewed TS requirements and
These activities were selected based on their potential risk significance relative to the  
      walked down portions of redundant safety systems, when applicable, to verify risk
Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that  
      analysis assumptions were valid and applicable requirements were met.
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
      These maintenance risk assessments and emergent work control activities constituted
and complete. When emergent work was performed, the inspectors verified that the  
      one sample as defined in IP 71111.13-05.
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
  b. Findings
of maintenance work, discussed the results of the assessment with the licensee's  
      No findings of significance were identified.
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
1R15 Operability Evaluations (71111.15)
consistent with the risk assessment. The inspectors also reviewed TS requirements and  
.1   Valve 2SI-897B Failure to Operate
walked down portions of redundant safety systems, when applicable, to verify risk  
  a. Inspection Scope
analysis assumptions were valid and applicable requirements were met.  
      The inspectors reviewed AR 01158812, written due to the failure of the 2SI-897B valve
These maintenance risk assessments and emergent work control activities constituted  
      to operate during test procedure IT 215, "SI Valves - Cold Shutdown."
one sample as defined in IP 71111.13-05.  
      The inspectors selected this potential operability issue based on the risk significance of
b.  
      the associated components and systems. The inspectors evaluated the technical
Findings  
      adequacy of the evaluations to ensure that TS past-operability and system functionality
No findings of significance were identified.  
                                                16                                        Enclosure
1R15 Operability Evaluations (71111.15)  
.1  
Valve 2SI-897B Failure to Operate  
a.  
Inspection Scope  
The inspectors reviewed AR 01158812, written due to the failure of the 2SI-897B valve  
to operate during test procedure IT 215, "SI Valves - Cold Shutdown."  
The inspectors selected this potential operability issue based on the risk significance of  
the associated components and systems. The inspectors evaluated the technical  
adequacy of the evaluations to ensure that TS past-operability and system functionality  


  were properly justified and the subject component or system remained available such
  that no unrecognized increase in risk occurred. The inspectors compared the operability
Enclosure
  and design criteria in the appropriate sections of the TSs and FSAR to the licensee's
17
  evaluations to determine whether the components or systems were operable or
were properly justified and the subject component or system remained available such  
  functional. The inspectors determined, where appropriate, compliance with bounding
that no unrecognized increase in risk occurred. The inspectors compared the operability  
  limitations associated with the evaluations. Additionally, the inspectors also reviewed a
and design criteria in the appropriate sections of the TSs and FSAR to the licensee's  
  sampling of corrective action documents to verify that the licensee was identifying and
evaluations to determine whether the components or systems were operable or  
  correcting any deficiencies associated with operability evaluations. Documents reviewed
functional. The inspectors determined, where appropriate, compliance with bounding  
  are listed in the Attachment to this report.
limitations associated with the evaluations. Additionally, the inspectors also reviewed a  
  This operability inspection constituted one sample as defined in IP 71111.15-05.
sampling of corrective action documents to verify that the licensee was identifying and  
b. Findings
correcting any deficiencies associated with operability evaluations. Documents reviewed  
  Failure to Ensure Adequate Control of Foreign Material in Safety-Related Systems
are listed in the Attachment to this report.  
  Introduction: A self-revealed finding of very low safety significance (Green) and
This operability inspection constituted one sample as defined in IP 71111.15-05.  
  associated Non-Cited Violation (NCV) of 10 CFR Part 50, Appendix B, Criterion V,
b.  
  "Instructions, Procedures and Drawings," was identified for the failure to ensure
Findings  
  adequate control of foreign material in accordance with the requirements of procedure
Failure to Ensure Adequate Control of Foreign Material in Safety-Related Systems  
  NP 8.4.10, "Exclusion of Foreign Material from Plant Components and Systems."
Introduction: A self-revealed finding of very low safety significance (Green) and  
  Description: On October 17, 2009, foreign material was discovered inside the 2SI-897B
associated Non-Cited Violation (NCV) of 10 CFR Part 50, Appendix B, Criterion V,  
  valve after the valve failed to properly stroke closed during the performance of test
"Instructions, Procedures and Drawings," was identified for the failure to ensure  
  procedure IT-215, "SI Valves - Cold Shutdown." Due to the tight clearances in the valve
adequate control of foreign material in accordance with the requirements of procedure  
  internals, once the foreign material became lodged in the valve trim cage, the valve plug
NP 8.4.10, "Exclusion of Foreign Material from Plant Components and Systems."  
  became stuck while it was being stroked. Upon retrieval of the material by the licensee,
Description: On October 17, 2009, foreign material was discovered inside the 2SI-897B  
  it was discovered to be a pliable, black nylon material about 1/2-inch wide by 5-inches
valve after the valve failed to properly stroke closed during the performance of test  
  long, and appeared to be a cable-tie of unknown origin or variety. The licensee
procedure IT-215, "SI Valves - Cold Shutdown." Due to the tight clearances in the valve  
  performed a boroscope inspection of the upstream and downstream piping for additional
internals, once the foreign material became lodged in the valve trim cage, the valve plug  
  fragments of the material and none were found. The licensee performed a Condition
became stuck while it was being stroked. Upon retrieval of the material by the licensee,  
  Evaluation, AR 01158812, to determine the most likely source of the material.
it was discovered to be a pliable, black nylon material about 1/2-inch wide by 5-inches  
  The licensee concluded that the material most likely was introduced into the Unit 2
long, and appeared to be a cable-tie of unknown origin or variety. The licensee  
  refueling water storage tank (RWST) where it flowed through a single-stage containment
performed a boroscope inspection of the upstream and downstream piping for additional  
  spray pump during testing to the safety injection (SI) pump test recirculation line.
fragments of the material and none were found. The licensee performed a Condition  
  The licensee also concluded that due to the pliable nature of the material, it was highly
Evaluation, AR 01158812, to determine the most likely source of the material.
  unlikely that the material would have damaged any pumps in its possible flow path.
The licensee concluded that the material most likely was introduced into the Unit 2  
  Valve 2SI-897B is one of two normally-open, redundant, AOVs in series with valve
refueling water storage tank (RWST) where it flowed through a single-stage containment  
  2SI-897A on the common Unit 2 SI pumps' test recirculation line (minimum-flow) to the
spray pump during testing to the safety injection (SI) pump test recirculation line.
  RWST. Together, these normally-open valves perform the safety function to remain
The licensee also concluded that due to the pliable nature of the material, it was highly  
  open during the SI injection phase to provide a minimum flow recirculation path to
unlikely that the material would have damaged any pumps in its possible flow path.  
  prevent damage to the SI pumps as a result of operating in a low flow or dead-headed
Valve 2SI-897B is one of two normally-open, redundant, AOVs in series with valve  
  condition. Since these valves were open, as designed, during modes in which the
2SI-897A on the common Unit 2 SI pumps' test recirculation line (minimum-flow) to the  
  SI system was required to be operable, this safety-function, and the operability of the
RWST. Together, these normally-open valves perform the safety function to remain  
  SI pumps was not impacted by this foreign material event.
open during the SI injection phase to provide a minimum flow recirculation path to  
  The SI-897A and B valves also have a safety function to manually close during the
prevent damage to the SI pumps as a result of operating in a low flow or dead-headed  
  transition from the injection phase of SI to the sump recirculation phase to prevent the
condition. Since these valves were open, as designed, during modes in which the  
  flow of recirculation coolant into the RWST and potentially release radioactivity via the
SI system was required to be operable, this safety-function, and the operability of the  
  RWST's open vent. During a small-break loss of coolant accident scenario, the
SI pumps was not impacted by this foreign material event.  
                                            17                                      Enclosure
The SI-897A and B valves also have a safety function to manually close during the  
transition from the injection phase of SI to the sump recirculation phase to prevent the  
flow of recirculation coolant into the RWST and potentially release radioactivity via the  
RWST's open vent. During a small-break loss of coolant accident scenario, the  


RHR pumps would take suction from the containment sump during the recirculation
phase and may be required to supply the SI pumps. If both SI-897A and B could not
Enclosure
close at that time, containment sump water would be lost to the RWST via the
18
minimum-flow line from the SI pumps, and radioactivity could be released to
RHR pumps would take suction from the containment sump during the recirculation  
atmosphere. It was this safety function that was affected when the foreign material
phase and may be required to supply the SI pumps. If both SI-897A and B could not  
caused the mechanical binding of the 2SI-897B valve's internals and caused the valve to
close at that time, containment sump water would be lost to the RWST via the  
bind when 75 percent shut during the performance of IT-215 on October 17. However,
minimum-flow line from the SI pumps, and radioactivity could be released to  
since the 2SI-897A valve stroked satisfactorily on October 17, the safety function was
atmosphere. It was this safety function that was affected when the foreign material  
maintained by this redundant valve. The last time that the 2SI-897B valve was
caused the mechanical binding of the 2SI-897B valve's internals and caused the valve to  
successfully stroked was May 3, 2008, during the previous performance of IT-215.
bind when 75 percent shut during the performance of IT-215 on October 17. However,  
Additionally, once these valves are required to shut during an accident scenario, there
since the 2SI-897A valve stroked satisfactorily on October 17, the safety function was  
are no sequences in which the valves would be required to re-open.
maintained by this redundant valve. The last time that the 2SI-897B valve was  
Analysis: The inspectors determined that the failure to ensure adequate control of
successfully stroked was May 3, 2008, during the previous performance of IT-215.
foreign material in safety-related systems was contrary to the requirements of
Additionally, once these valves are required to shut during an accident scenario, there  
procedure NP 8.4.10, "Exclusion of Foreign Material from Plant Components and
are no sequences in which the valves would be required to re-open.  
Systems," and was a performance deficiency.
Analysis: The inspectors determined that the failure to ensure adequate control of  
The finding was determined to be more than minor because it was associated with the
foreign material in safety-related systems was contrary to the requirements of  
Barrier Integrity Cornerstone attribute of human performance and adversely affected the
procedure NP 8.4.10, "Exclusion of Foreign Material from Plant Components and  
associated cornerstone objective of providing reasonable assurance that physical design
Systems," and was a performance deficiency.  
barriers protect the public from radionuclide releases caused by accidents or events.
The finding was determined to be more than minor because it was associated with the  
Specifically, due to the interference caused by the foreign material inside the 2SI-897B
Barrier Integrity Cornerstone attribute of human performance and adversely affected the  
valve, the valve would not have been able to perform its safety function to close during
associated cornerstone objective of providing reasonable assurance that physical design  
the initiation of the post-LOCA sump-recirculation phase of safety injection.
barriers protect the public from radionuclide releases caused by accidents or events.
The inspectors determined the finding could be evaluated in accordance with IMC 0609,
Specifically, due to the interference caused by the foreign material inside the 2SI-897B  
Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening
valve, the valve would not have been able to perform its safety function to close during  
and Characterization of Findings, Table 4a, containment barrier column, dated
the initiation of the post-LOCA sump-recirculation phase of safety injection.  
January 10, 2008. The finding was determined to be of very low safety significance
The inspectors determined the finding could be evaluated in accordance with IMC 0609,  
(Green) because the issue did not represent a degradation of the radiological barrier
Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening  
function provided for the control room, or auxiliary building, or spent fuel pool; represent
and Characterization of Findings, Table 4a, containment barrier column, dated  
a degradation of the barrier function of the control room against smoke or a toxic
January 10, 2008. The finding was determined to be of very low safety significance  
atmosphere; represent an actual open pathway in the physical integrity of reactor
(Green) because the issue did not represent a degradation of the radiological barrier  
containment (valves, airlocks, containment isolation system (logic and instrumentation)),
function provided for the control room, or auxiliary building, or spent fuel pool; represent  
and heat removal components; nor involve an actual reduction in function of hydrogen
a degradation of the barrier function of the control room against smoke or a toxic  
ignitors in the reactor containment. No cross-cutting aspect was identified because the
atmosphere; represent an actual open pathway in the physical integrity of reactor  
foreign material was determined to have been introduced into the system in the past and
containment (valves, airlocks, containment isolation system (logic and instrumentation)),  
was not considered indicative of current performance.
and heat removal components; nor involve an actual reduction in function of hydrogen  
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
ignitors in the reactor containment. No cross-cutting aspect was identified because the  
and Drawings, requires, in part, that activities affecting quality be prescribed by
foreign material was determined to have been introduced into the system in the past and  
documented instructions, procedures, or drawings, of a type appropriate to the
was not considered indicative of current performance.  
circumstances and shall be accomplished in accordance with these instructions,
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
procedures, or drawings. Specifically, procedure NP 8.4.10, required, in part, that
and Drawings, requires, in part, that activities affecting quality be prescribed by  
maintenance activities preclude the introduction of foreign material into the SI system.
documented instructions, procedures, or drawings, of a type appropriate to the  
Contrary to this, prior to October 17, 2009, the licensee failed to accomplish activities
circumstances and shall be accomplished in accordance with these instructions,  
affecting the quality of the SI system in accordance with the documented instructions
procedures, or drawings. Specifically, procedure NP 8.4.10, required, in part, that  
and procedures associated with the exclusion of foreign material from safety-related
maintenance activities preclude the introduction of foreign material into the SI system.  
plant equipment and systems, an activity affecting quality. Specifically, during a
Contrary to this, prior to October 17, 2009, the licensee failed to accomplish activities  
                                          18                                        Enclosure
affecting the quality of the SI system in accordance with the documented instructions  
and procedures associated with the exclusion of foreign material from safety-related  
plant equipment and systems, an activity affecting quality. Specifically, during a  


    previous work activity involving an open safety-related fluid system boundary, such as
    the RWST, the licensee failed to adequately control foreign material in accordance with
Enclosure
    procedure NP 8.4.10. Because this violation was of very low safety significance and
19
    was entered into the licensees CAP as AR 011588112, "2SI897B Failed to Operate,"
previous work activity involving an open safety-related fluid system boundary, such as  
    this violation is being treated as an NCV, consistent with Section VI.A.1 of the
the RWST, the licensee failed to adequately control foreign material in accordance with  
    NRC Enforcement Policy (NCV 05000301/2009005-02).
procedure NP 8.4.10. Because this violation was of very low safety significance and  
    In response to this issue, the licensee took prompt corrective actions to repair the valve
was entered into the licensees CAP as AR 011588112, "2SI897B Failed to Operate,"  
    and perform an extent-of-condition review, including a boroscope inspection of the
this violation is being treated as an NCV, consistent with Section VI.A.1 of the  
    upstream and downstream piping. Additionally, upon entering the issue into its CAP, the
NRC Enforcement Policy (NCV 05000301/2009005-02).  
    licensee performed a causal evaluation to determine the most probable location through
In response to this issue, the licensee took prompt corrective actions to repair the valve  
    which the foreign material entered and to develop appropriate corrective actions.
and perform an extent-of-condition review, including a boroscope inspection of the  
.2   Operability Evaluations
upstream and downstream piping. Additionally, upon entering the issue into its CAP, the  
  a. Inspection Scope
licensee performed a causal evaluation to determine the most probable location through  
    The inspectors reviewed the following issues:
which the foreign material entered and to develop appropriate corrective actions.  
    *       AR 01161636; New Auxiliary Feedwater Line in Contact with Service Water Pipe;
.2  
    *       AR 01160262; 1HX-I5C CFC Flow Out-of-Limit Low per TS-33;
Operability Evaluations  
    *       AR 01158549; U2R20 Mode 3 UT [ultrasonic testing] Results - GL 08-01; and
a.  
    *       AR 01159784; Spent Fuel Pool Pump Suction Isolation Valve Stem Contacting
Inspection Scope  
              Adjacent Pipe Insulation.
The inspectors reviewed the following issues:  
    The inspectors selected this potential operability issue based on the risk significance of
*  
    the associated components and systems. The inspectors evaluated the technical
AR 01161636; New Auxiliary Feedwater Line in Contact with Service Water Pipe;  
    adequacy of the evaluations to ensure that TS operability and system functionality were
*  
    properly justified and the subject component or system remained available such that no
AR 01160262; 1HX-I5C CFC Flow Out-of-Limit Low per TS-33;  
    unrecognized increase in risk occurred. The inspectors compared the operability and
*  
    design criteria in the appropriate sections of the TSs and FSAR to the licensee's
AR 01158549; U2R20 Mode 3 UT [ultrasonic testing] Results - GL 08-01; and  
    evaluations to determine whether the components or systems were operable or
*  
    functional. Where compensatory measures were required to maintain operability, the
AR 01159784; Spent Fuel Pool Pump Suction Isolation Valve Stem Contacting  
    inspectors determined whether the measures in place would function as intended and
Adjacent Pipe Insulation.  
    were properly controlled. The inspectors determined, where appropriate, compliance
The inspectors selected this potential operability issue based on the risk significance of  
    with bounding limitations associated with the evaluations. Additionally, the inspectors
the associated components and systems. The inspectors evaluated the technical  
    also reviewed a sampling of corrective action documents to verify that the licensee was
adequacy of the evaluations to ensure that TS operability and system functionality were  
    identifying and correcting any deficiencies associated with operability evaluations.
properly justified and the subject component or system remained available such that no  
    Documents reviewed are listed in the Attachment to this report.
unrecognized increase in risk occurred. The inspectors compared the operability and  
    This operability inspection constituted four samples as defined in IP 71111.15-05.
design criteria in the appropriate sections of the TSs and FSAR to the licensee's  
  b. Findings
evaluations to determine whether the components or systems were operable or  
    No findings of significance were identified.
functional. Where compensatory measures were required to maintain operability, the  
                                              19                                      Enclosure
inspectors determined whether the measures in place would function as intended and  
were properly controlled. The inspectors determined, where appropriate, compliance  
with bounding limitations associated with the evaluations. Additionally, the inspectors  
also reviewed a sampling of corrective action documents to verify that the licensee was  
identifying and correcting any deficiencies associated with operability evaluations.
Documents reviewed are listed in the Attachment to this report.  
This operability inspection constituted four samples as defined in IP 71111.15-05.  
b.  
Findings  
No findings of significance were identified.  


1R18 Plant Modifications (71111.18)
.1   Temporary Plant Modifications
Enclosure
  a. Inspection Scope
20
      The inspectors reviewed the following temporary modification:
1R18 Plant Modifications (71111.18)  
      *       modifications in Unit 2 turbine building to facilitate installation of new feedwater
.1  
              heaters.
Temporary Plant Modifications  
      The inspectors compared the temporary configuration changes and associated
a.  
      10 CFR 50.59 screening and evaluation information against the design basis, the FSAR,
Inspection Scope  
      and the TSs, as applicable, to verify that the modification did not affect the operability or
The inspectors reviewed the following temporary modification:  
      availability of the affected systems. The inspectors also compared the licensee's
*  
      information to operating experience information to ensure that lessons learned from
modifications in Unit 2 turbine building to facilitate installation of new feedwater  
      other utilities had been incorporated into the licensee's decision to implement the
heaters.  
      temporary modification. The inspectors, as applicable, performed field verifications to
The inspectors compared the temporary configuration changes and associated  
      ensure that the modifications were installed as directed; the modifications operated as
10 CFR 50.59 screening and evaluation information against the design basis, the FSAR,  
      expected; modification testing adequately demonstrated continued system operability,
and the TSs, as applicable, to verify that the modification did not affect the operability or  
      availability, and reliability; and that operation of the modifications did not impact the
availability of the affected systems. The inspectors also compared the licensee's  
      operability of any interfacing systems. Lastly, the inspectors discussed the temporary
information to operating experience information to ensure that lessons learned from  
      modification with operations, engineering. Documents reviewed are listed in the
other utilities had been incorporated into the licensee's decision to implement the  
      Attachment to this report.
temporary modification. The inspectors, as applicable, performed field verifications to  
      This inspection constituted one temporary modification sample as defined in
ensure that the modifications were installed as directed; the modifications operated as  
      IP 71111.18-05.
expected; modification testing adequately demonstrated continued system operability,  
  b. Findings
availability, and reliability; and that operation of the modifications did not impact the  
      Failure to Update Safe Load Path Manual to Include Safety-Related Cable Locations
operability of any interfacing systems. Lastly, the inspectors discussed the temporary  
      Introduction: A finding of very low safety significance and associated NCV of
modification with operations, engineering. Documents reviewed are listed in the  
      10 CFR Part 50, Appendix B, Criterion III, "Design Control," was identified for the failure
Attachment to this report.  
      to ensure that the safe load path (SLP) and rigging manual for the Unit 2 turbine building
This inspection constituted one temporary modification sample as defined in  
      crane (SLP-3), was updated as part of the major safety-related modification that added
IP 71111.18-05.  
      the G-03 and G-04 EDGs in 1995 and 1996.
b.  
      Description: On October 14, 2009, the licensee generated AR 1158472, which captured
Findings  
      an NRC-identified concern regarding the adequacy of SLP-3 with respect to the G-03
Failure to Update Safe Load Path Manual to Include Safety-Related Cable Locations  
      and G-04 modifications. Specifically, it was identified that SLP-3 allowed unrestricted
Introduction: A finding of very low safety significance and associated NCV of  
      load lifts over the U2 turbine building truck-bay area based upon evaluations performed
10 CFR Part 50, Appendix B, Criterion III, "Design Control," was identified for the failure  
      in the early 1980s in response to NRC GL 81-07 "Control of Heavy Loads," and was not
to ensure that the safe load path (SLP) and rigging manual for the Unit 2 turbine building  
      updated to reflect changes to the design of the facility when the G-03 and G-04 EDGs
crane (SLP-3), was updated as part of the major safety-related modification that added  
      were installed and a modification added safety-related, risk-significant, cables under the
the G-03 and G-04 EDGs in 1995 and 1996.  
      Unit 2 truck bay in 1995 and 1996. These cables included the 4160-volt AC output
Description: On October 14, 2009, the licensee generated AR 1158472, which captured  
      cables from the train B EDGs (G-03 and G-04), and the 480-volt AC power cables to
an NRC-identified concern regarding the adequacy of SLP-3 with respect to the G-03  
      the train A EDGs (G-01 and G-02) fuel oil transfer pumps. Due to the close proximity
and G-04 modifications. Specifically, it was identified that SLP-3 allowed unrestricted  
      of A and B train cables, a loss of both trains of emergency AC power could result if
load lifts over the U2 turbine building truck-bay area based upon evaluations performed  
      the underground cables were disabled by a postulated dropped load of sufficient
in the early 1980s in response to NRC GL 81-07 "Control of Heavy Loads," and was not  
                                                  20                                        Enclosure
updated to reflect changes to the design of the facility when the G-03 and G-04 EDGs  
were installed and a modification added safety-related, risk-significant, cables under the  
Unit 2 truck bay in 1995 and 1996. These cables included the 4160-volt AC output  
cables from the train B EDGs (G-03 and G-04), and the 480-volt AC power cables to  
the train A EDGs (G-01 and G-02) fuel oil transfer pumps. Due to the close proximity  
of A and B train cables, a loss of both trains of emergency AC power could result if  
the underground cables were disabled by a postulated dropped load of sufficient  


magnitude, such as a drop of the spare low pressure turbine rotor from the 66-foot
elevation.
Enclosure
On September 30, 2009, the inspectors initially queried the licensee about upcoming
21
Unit 2 feedwater (FW) heater replacement activities, with heavy load lifts scheduled for
magnitude, such as a drop of the spare low pressure turbine rotor from the 66-foot  
the Unit 2 truck bay during the fall 2009 RFO. Specifically, the inspectors inquired about
elevation.  
the underground cables and whether or not the licensee had accounted for them in the
On September 30, 2009, the inspectors initially queried the licensee about upcoming  
preparations for the FW heater removals and installations with regard to potential load
Unit 2 feedwater (FW) heater replacement activities, with heavy load lifts scheduled for  
drop effects. When the inspectors asked for the licensee's justification for why a load
the Unit 2 truck bay during the fall 2009 RFO. Specifically, the inspectors inquired about  
drop analysis had not been performed, the licensee stated that it was unnecessary
the underground cables and whether or not the licensee had accounted for them in the  
because SLP-3 allowed for unrestricted load lifts in that area.
preparations for the FW heater removals and installations with regard to potential load  
When the inspectors examined the basis for SLP-3, it was noted that the plan for that
drop effects. When the inspectors asked for the licensee's justification for why a load  
area had remained essentially unchanged since its initial creation in the early 1980s,
drop analysis had not been performed, the licensee stated that it was unnecessary  
before the installation of the G-03 and G-04 EDGs in 1995 and 1996. It became evident
because SLP-3 allowed for unrestricted load lifts in that area.  
to the inspectors that the SLP-3 had not been sufficiently revised to account for the
When the inspectors examined the basis for SLP-3, it was noted that the plan for that  
existence of the risk-significant cables under the Unit 2 truck bay.
area had remained essentially unchanged since its initial creation in the early 1980s,  
As a result of these discussions, the licensee determined that a 2 inch-thick layer of steel
before the installation of the G-03 and G-04 EDGs in 1995 and 1996. It became evident  
plates would be temporarily installed under the FW heater load lift area to provide
to the inspectors that the SLP-3 had not been sufficiently revised to account for the  
adequate protection for the cables in the event of a load drop.
existence of the risk-significant cables under the Unit 2 truck bay.  
Analysis: The inspectors determined that the failure to update the SLP-3 as a part of the
As a result of these discussions, the licensee determined that a 2 inch-thick layer of steel  
engineering change process when the diesel generator modification was implemented
plates would be temporarily installed under the FW heater load lift area to provide  
was contrary to the requirements of 10 CFR Part 50, Appendix B, Criterion III,
adequate protection for the cables in the event of a load drop.  
"Design Control," and was a performance deficiency.
Analysis: The inspectors determined that the failure to update the SLP-3 as a part of the  
The finding was more than minor because it was associated with the Mitigating Systems
engineering change process when the diesel generator modification was implemented  
Cornerstone attribute of design control and adversely affected the associated
was contrary to the requirements of 10 CFR Part 50, Appendix B, Criterion III,  
cornerstone objective of ensuring the availability, reliability, and capability of systems
"Design Control," and was a performance deficiency.  
that respond to initiating events to prevent undesirable consequences (i.e., core
The finding was more than minor because it was associated with the Mitigating Systems  
damage). In accordance with NRC IMC 0609, Appendix A, "Significance Determination
Cornerstone attribute of design control and adversely affected the associated  
of Reactor Inspection Findings for At-Power Situations," dated January 10, 2008, the
cornerstone objective of ensuring the availability, reliability, and capability of systems  
inspectors conducted a Phase 1 SDP screening and determined the finding to be of very
that respond to initiating events to prevent undesirable consequences (i.e., core  
low safety significance (Green) because the finding was not a design or qualification
damage). In accordance with NRC IMC 0609, Appendix A, "Significance Determination  
deficiency, did not represent a loss of system safety function or loss of a single train for
of Reactor Inspection Findings for At-Power Situations," dated January 10, 2008, the  
greater than its allowed technical specification time, and did not screen as potentially
inspectors conducted a Phase 1 SDP screening and determined the finding to be of very  
risk-significant due to seismic, flooding, or severe weather initiating events.
low safety significance (Green) because the finding was not a design or qualification  
This finding has a cross-cutting aspect in the area of problem identification and
deficiency, did not represent a loss of system safety function or loss of a single train for  
resolution, CAP, because the staff did not take appropriate corrective actions to address
greater than its allowed technical specification time, and did not screen as potentially  
safety issues in a timely manner, commensurate with their safety significance.
risk-significant due to seismic, flooding, or severe weather initiating events.  
Specifically, when AR 1122278 from February 2008 raised similar questions regarding
This finding has a cross-cutting aspect in the area of problem identification and  
the adequacy of SLP-3, no revision to the SLP resulted, despite one being drafted at the
resolution, CAP, because the staff did not take appropriate corrective actions to address  
time. That AR was closed in April 2009 to no actions taken. Inspectors viewed that AR
safety issues in a timely manner, commensurate with their safety significance.
as a missed opportunity for the site to resolve the SLP-3 issue (P.1(d)).
Specifically, when AR 1122278 from February 2008 raised similar questions regarding  
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,
the adequacy of SLP-3, no revision to the SLP resulted, despite one being drafted at the  
in part, that measures be established to assure that applicable regulatory requirements
time. That AR was closed in April 2009 to no actions taken. Inspectors viewed that AR  
and the design basis are correctly translated into specifications, drawings, procedures,
as a missed opportunity for the site to resolve the SLP-3 issue (P.1(d)).  
and instructions. Contrary to this, from initial in-service installation of the G-03 and G-04
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,  
                                          21                                        Enclosure
in part, that measures be established to assure that applicable regulatory requirements  
and the design basis are correctly translated into specifications, drawings, procedures,  
and instructions. Contrary to this, from initial in-service installation of the G-03 and G-04  


    EDGs, to the point when SLP-3 was corrected in October 2009, the licensee failed to
    ensure that the design bases changes to the EDG system were correctly translated into
Enclosure
    specifications, drawings, procedures, and instructions. Because this violation was of
22
    very low safety significance and was entered into the licensees CAP, as AR 1158472,
EDGs, to the point when SLP-3 was corrected in October 2009, the licensee failed to  
    this violation is being treated as an NCV, consistent with Section VI.A.1 of the
ensure that the design bases changes to the EDG system were correctly translated into  
    NRC Enforcement Policy (NCV 05000301/2009005-03).
specifications, drawings, procedures, and instructions. Because this violation was of  
    The licensee's corrective actions addressed the immediate concern by installing
very low safety significance and was entered into the licensees CAP, as AR 1158472,  
    temporary steel plates over the affected area of the truck bay to provide adequate
this violation is being treated as an NCV, consistent with Section VI.A.1 of the  
    protection for upcoming heavy load lifts. Additionally, the licensee revised SLP-3 to
NRC Enforcement Policy (NCV 05000301/2009005-03).  
    require additional risk mitigation measures be taken prior to any future heavy load lifts in
The licensee's corrective actions addressed the immediate concern by installing  
    that area.
temporary steel plates over the affected area of the truck bay to provide adequate  
.2   Permanent Plant Modifications
protection for upcoming heavy load lifts. Additionally, the licensee revised SLP-3 to  
  a. Inspection Scope
require additional risk mitigation measures be taken prior to any future heavy load lifts in  
    The following engineering design packages were reviewed and selected aspects were
that area.  
    discussed with engineering personnel:
.2  
    *       GSI 191 (Generic Safety Issue) modifications EC [Engineering Change] 13601 -
Permanent Plant Modifications  
              RCP [Reactor Coolant Pump] S/G, and RCS Loops Piping Insulation
a.  
              Replacement - Unit 2, and EC 12601 - Additional Sump Strainer Modules -
Inspection Scope  
              Unit 2; and
The following engineering design packages were reviewed and selected aspects were  
    *       EC 11542; Unit 2 Main Generator Circuit Breaker Addition.
discussed with engineering personnel:  
    These documents and related documentation were reviewed for adequacy of the
*  
    associated 10 CFR 50.59 safety evaluation screening, consideration of design
GSI 191 (Generic Safety Issue) modifications EC [Engineering Change] 13601 -  
    parameters, implementation of the modification, post-modification testing, and proper
RCP [Reactor Coolant Pump] S/G, and RCS Loops Piping Insulation  
    update of relevant procedures, design, and licensing documents. The inspectors
Replacement - Unit 2, and EC 12601 - Additional Sump Strainer Modules -  
    observed ongoing and completed work activities to verify that installation was consistent
Unit 2; and  
    with the design control documents. The first sample was for the modification that
*  
    replaced the Unit 2 main generator circuit breaker, and the other sample was for
EC 11542; Unit 2 Main Generator Circuit Breaker Addition.  
    GSI-191 modifications in the Unit 2 containment that replaced insulation and added
These documents and related documentation were reviewed for adequacy of the  
    additional sump strainer modules. Documents reviewed are listed in the Attachment to
associated 10 CFR 50.59 safety evaluation screening, consideration of design  
    this report.
parameters, implementation of the modification, post-modification testing, and proper  
    Specifically, the inspectors conducted a walkdown of the strainer assemblies during the
update of relevant procedures, design, and licensing documents. The inspectors  
    fall 2009 RFO for Unit 2. The engineering design packages were associated with the
observed ongoing and completed work activities to verify that installation was consistent  
    licensee's response to GL 2004-02, "Potential Impact of Debris Blockage on Emergency
with the design control documents. The first sample was for the modification that  
    Recirculation During Design Basis Accidents at Pressurized-Water Reactors."
replaced the Unit 2 main generator circuit breaker, and the other sample was for  
    The licensee's implementation of commitments documented in its initial responses to
GSI-191 modifications in the Unit 2 containment that replaced insulation and added  
    GL 2004-02 was previously reviewed in accordance with temporary instruction
additional sump strainer modules. Documents reviewed are listed in the Attachment to  
    (TI) 2515/166, "Pressurized Water Reactor Containment Sump Blockage." The
this report.  
    closure of this TI in the summer 2008, documented in NRC Inspection Report (IR)
Specifically, the inspectors conducted a walkdown of the strainer assemblies during the  
    05000266/2008003; 05000301/2008003, indicated that the licensee had received
fall 2009 RFO for Unit 2. The engineering design packages were associated with the  
    approval for an extension for GL 2004-02 corrective actions.
licensee's response to GL 2004-02, "Potential Impact of Debris Blockage on Emergency  
    In July 2008, after the establishment of an industry head loss test protocol, the licensee
Recirculation During Design Basis Accidents at Pressurized-Water Reactors."
    conducted additional testing using the revised test methodologies. During this testing,
The licensee's implementation of commitments documented in its initial responses to  
    the licensee determined that the original containment sump strainer modification of
GL 2004-02 was previously reviewed in accordance with temporary instruction  
                                              22                                      Enclosure
(TI) 2515/166, "Pressurized Water Reactor Containment Sump Blockage." The  
closure of this TI in the summer 2008, documented in NRC Inspection Report (IR)  
05000266/2008003; 05000301/2008003, indicated that the licensee had received  
approval for an extension for GL 2004-02 corrective actions.  
In July 2008, after the establishment of an industry head loss test protocol, the licensee  
conducted additional testing using the revised test methodologies. During this testing,  
the licensee determined that the original containment sump strainer modification of  


  11 strainer modules per train, which had already been installed, did not meet test
  acceptance criteria. As a result, the licensee installed three additional strainers modules
Enclosure
  per train, added debris interceptors, removed fibrous insulation in the fall 2008 RFO for
23
  Unit 1, and planned similar modifications for the fall 2009 RFO for Unit 2. The purpose
11 strainer modules per train, which had already been installed, did not meet test  
  of the modification was to obtain additional net positive suction head margin for the
acceptance criteria. As a result, the licensee installed three additional strainers modules  
  residual heat removal pumps. However, prototypical testing of the debris interceptors in
per train, added debris interceptors, removed fibrous insulation in the fall 2008 RFO for  
  January 2009 indicated that the efficiency of the debris interceptors was not as high as
Unit 1, and planned similar modifications for the fall 2009 RFO for Unit 2. The purpose  
  required. In order to address this issue and recent concerns regarding the assumed
of the modification was to obtain additional net positive suction head margin for the  
  destruction zone of influence for fibrous insulation, the licensee planned to remove
residual heat removal pumps. However, prototypical testing of the debris interceptors in  
  additional fibrous insulation and revise the debris generation and transport analyses
January 2009 indicated that the efficiency of the debris interceptors was not as high as  
  accordingly. Specifically, the licensee developed an additional modification that reduced
required. In order to address this issue and recent concerns regarding the assumed  
  the amount of fibrous insulation debris by replacing the existing insulation with metallic
destruction zone of influence for fibrous insulation, the licensee planned to remove  
  reflective insulation on reactor coolant pumps bowl assemblies, portions of steam
additional fibrous insulation and revise the debris generation and transport analyses  
  generators, and portions of reactor coolant system loop piping.
accordingly. Specifically, the licensee developed an additional modification that reduced  
  The licensee requested and received NRC approval for an extension for GL 2004-02
the amount of fibrous insulation debris by replacing the existing insulation with metallic  
  corrective actions to June 30, 2010, for Unit 1, and June 20, 2011, for Unit 2. Since the
reflective insulation on reactor coolant pumps bowl assemblies, portions of steam  
  closure of TI 2515/166, the licensee has completed the following actions:
generators, and portions of reactor coolant system loop piping.  
      *   installation of an additional three strainer modules per train to increase the
The licensee requested and received NRC approval for an extension for GL 2004-02  
            overall surface area in Units 1 and 2;
corrective actions to June 30, 2010, for Unit 1, and June 20, 2011, for Unit 2. Since the  
      *   installation of debris interceptors to reduce the quantity of suspended debris that
closure of TI 2515/166, the licensee has completed the following actions:  
            could be transported to the screen surface in Unit 1;
*  
      *   structural reinforcement of the strainer assemblies to accommodate an increased
installation of an additional three strainer modules per train to increase the  
            differential pressure in Unit 2;
overall surface area in Units 1 and 2;  
      *   extension of the refueling cavity drain line away from the strainers in order to
*  
            prevent water from spilling on or near the strainers and potentially causing air
installation of debris interceptors to reduce the quantity of suspended debris that  
            ingestion in Units 1 and 2; and
could be transported to the screen surface in Unit 1;  
      *   initiated the fibrous insulation reduction effort in Units 1 and 2.
*  
  The outstanding actions are:
structural reinforcement of the strainer assemblies to accommodate an increased  
      *   complete the fibrous insulation reduction effort during the spring 2010 RFO for
differential pressure in Unit 2;  
            Unit 1 and the spring 2011 RFO for Unit 2; and
*  
      *   update the licensing bases as required.
extension of the refueling cavity drain line away from the strainers in order to  
  This inspection constituted two permanent plant modification samples as defined in
prevent water from spilling on or near the strainers and potentially causing air  
  IP 71111.18-05.
ingestion in Units 1 and 2; and  
b. Findings
*  
  Potential Failure To Adequately Evaluate Seismic II/I Concerns For Units 1 And 2
initiated the fibrous insulation reduction effort in Units 1 and 2.  
  B Containment Sump Strainers
The outstanding actions are:  
  Introduction: The inspectors identified an unresolved item (URI) regarding the B
*  
  containment sump strainers for Units 1 and 2. Specifically, the inspectors questioned
complete the fibrous insulation reduction effort during the spring 2010 RFO for  
                                              23                                      Enclosure
Unit 1 and the spring 2011 RFO for Unit 2; and  
*  
update the licensing bases as required.  
This inspection constituted two permanent plant modification samples as defined in  
IP 71111.18-05.  
b.  
Findings  
Potential Failure To Adequately Evaluate Seismic II/I Concerns For Units 1 And 2  
B Containment Sump Strainers  
Introduction: The inspectors identified an unresolved item (URI) regarding the B  
containment sump strainers for Units 1 and 2. Specifically, the inspectors questioned  


whether the ventilation ducts located above containment sump strainers were
adequately evaluated with respect to seismic II/I considerations.
Enclosure
Description: On October 27, 2009, the inspectors performed a walkdown of the
24
containment sump strainers of Unit 2 and noted a ventilation duct located above the
whether the ventilation ducts located above containment sump strainers were  
B containment sump strainer. The inspectors were concerned that during a seismic
adequately evaluated with respect to seismic II/I considerations.  
event the structure could collapse and affect the strainers ability to fulfill its accident
Description: On October 27, 2009, the inspectors performed a walkdown of the  
mitigating function. Specifically, if the ventilation duct and its support structure
containment sump strainers of Unit 2 and noted a ventilation duct located above the  
collapsed, the structural integrity of the sump strainer could be compromised or the
B containment sump strainer. The inspectors were concerned that during a seismic  
failed duct and support could block the strainers. The sump strainers are relied upon to
event the structure could collapse and affect the strainers ability to fulfill its accident  
simultaneously maintain an adequate post-loss-of-coolant-accident suction source while
mitigating function. Specifically, if the ventilation duct and its support structure  
preventing debris from entering the emergency core cooling system.
collapsed, the structural integrity of the sump strainer could be compromised or the  
The licensee's immediate documentation search on the seismic evaluation of the
failed duct and support could block the strainers. The sump strainers are relied upon to  
ventilation duct was unsuccessful. The licensee initiated AR 01159937. The licensee
simultaneously maintain an adequate post-loss-of-coolant-accident suction source while  
also determined that the same condition existed in Unit 1 and performed a prompt
preventing debris from entering the emergency core cooling system.  
operability determination for the Unit 1 B strainer.
The licensee's immediate documentation search on the seismic evaluation of the  
The licensee later determined that the installation modification documentation for Unit 1,
ventilation duct was unsuccessful. The licensee initiated AR 01159937. The licensee  
Engineering Change (EC) 1602, indicated that the modification did not require analysis
also determined that the same condition existed in Unit 1 and performed a prompt  
of non-seismic components located over or adjacent to seismic components because
operability determination for the Unit 1 B strainer.  
there was no evidence of a potential seismic II/I concern at the time the modification was
The licensee later determined that the installation modification documentation for Unit 1,  
completed. Specifically, a seismic interaction walkdown was required in the installation
Engineering Change (EC) 1602, indicated that the modification did not require analysis  
work plan prior to the installation of the strainers. The walkdown was completed by two
of non-seismic components located over or adjacent to seismic components because  
civil engineers who were Seismic Qualification Users Group (SQUG) qualified.
there was no evidence of a potential seismic II/I concern at the time the modification was  
The licensee determined, through discussions with the engineers who performed the
completed. Specifically, a seismic interaction walkdown was required in the installation  
walkdown, that the ventilation ducts were reviewed. Based on these facts, the licensee
work plan prior to the installation of the strainers. The walkdown was completed by two  
concluded that: (1) the ventilation ducts were seismically evaluated; (2) the evaluation
civil engineers who were Seismic Qualification Users Group (SQUG) qualified.
determined that there are no seismic II/I concerns; and (3) that this is a documentation
The licensee determined, through discussions with the engineers who performed the  
issue. The same conclusions applied to Unit 2.
walkdown, that the ventilation ducts were reviewed. Based on these facts, the licensee  
However, the inspectors were concerned with the use of SQUG methodology to
concluded that: (1) the ventilation ducts were seismically evaluated; (2) the evaluation  
evaluate the seismic II/I interactions with respect to the duct ventilation and the strainer.
determined that there are no seismic II/I concerns; and (3) that this is a documentation  
Specifically, the inspectors questioned whether this methodology could be applied to
issue. The same conclusions applied to Unit 2.  
ventilation ducts because this type of structure did not appear in the equipment classes
However, the inspectors were concerned with the use of SQUG methodology to  
of the implementing procedure for SQUG. As a result of the inspectors' questions,
evaluate the seismic II/I interactions with respect to the duct ventilation and the strainer.
the licensee performed a prompt operability determination, in accordance with
Specifically, the inspectors questioned whether this methodology could be applied to  
EN-AA-203-1001 that determined the Unit 1 B sump strainer was operable. The
ventilation ducts because this type of structure did not appear in the equipment classes  
basis for this conclusion was documented in EC 14790. This EC performed a structural
of the implementing procedure for SQUG. As a result of the inspectors' questions,  
analysis that concluded that the ventilation duct support structure would be able to
the licensee performed a prompt operability determination, in accordance with  
support loads induced by a seismic event. Again, this evaluation applied to Unit 2.
EN-AA-203-1001 that determined the Unit 1 B sump strainer was operable. The  
In addition, the inspectors noted that the FSAR, Appendix A5.6, stated that
basis for this conclusion was documented in EC 14790. This EC performed a structural  
"Modified, new, or replacement equipment classified as Seismic Class I may be
analysis that concluded that the ventilation duct support structure would be able to  
seismically designed and verified (after installation) for seismic adequacy using seismic
support loads induced by a seismic event. Again, this evaluation applied to Unit 2.  
experience data in accordance with a methodology developed by the SQUG." It was not
In addition, the inspectors noted that the FSAR, Appendix A5.6, stated that  
clear whether this statement applied for all new modifications or to the replacement of
"Modified, new, or replacement equipment classified as Seismic Class I may be  
previously SQUG-qualified equipment with similar equipment.
seismically designed and verified (after installation) for seismic adequacy using seismic  
The inspectors were also concerned with the level of documentation maintained by the
experience data in accordance with a methodology developed by the SQUG." It was not  
licensee for the walkdowns performed using the SQUG methodology. Specifically, the
clear whether this statement applied for all new modifications or to the replacement of  
                                          24                                          Enclosure
previously SQUG-qualified equipment with similar equipment.  
The inspectors were also concerned with the level of documentation maintained by the  
licensee for the walkdowns performed using the SQUG methodology. Specifically, the  


      inspectors noted that the documentation did not provide the necessary details to permit
      independent auditing of the inferences or conclusions.
Enclosure
      This issue is unresolved pending further NRC review of the licensing basis for the use of
25
      SQUG methodology and determination of further NRC actions to resolve the issues
inspectors noted that the documentation did not provide the necessary details to permit  
      (URI 05000266/2009005-04; 05000301/2009005-04).
independent auditing of the inferences or conclusions.  
1R19 Post-Maintenance Testing (71111.19)
This issue is unresolved pending further NRC review of the licensing basis for the use of  
.1   Post-Maintenance Testing (PMT)
SQUG methodology and determination of further NRC actions to resolve the issues  
  a. Inspection Scope
(URI 05000266/2009005-04; 05000301/2009005-04).  
      The inspectors reviewed the following PMT activities to verify that procedures and test
1R19 Post-Maintenance Testing (71111.19)  
      activities were adequate to ensure system operability and functional capability:
.1  
      *       auxiliary feedwater and containment spray systems post-weld testing;
Post-Maintenance Testing (PMT)  
      *       TS-82 monthly EDG run PMT for annual maintenance and failed level switch in
a.  
              sump tank;
Inspection Scope  
      *       RHR pump 2P-10B PMT after oil leak repair; and
The inspectors reviewed the following PMT activities to verify that procedures and test  
      *       Unit 2 polar crane PMT following cable replacement.
activities were adequate to ensure system operability and functional capability:  
      These activities were selected based upon the structure, system, or component's ability
*  
      to impact risk. The inspectors evaluated these activities for the following (as applicable):
auxiliary feedwater and containment spray systems post-weld testing;  
      the effect of testing on the plant had been adequately addressed; testing was adequate
*  
      for the maintenance performed; acceptance criteria were clear and demonstrated
TS-82 monthly EDG run PMT for annual maintenance and failed level switch in  
      operational readiness; test instrumentation was appropriate; tests were performed as
sump tank;  
      written in accordance with properly reviewed and approved procedures; equipment was
*  
      returned to its operational status following testing (temporary modifications or jumpers
RHR pump 2P-10B PMT after oil leak repair; and  
      required for test performance were properly removed after test completion); and test
*  
      documentation was properly evaluated. The inspectors evaluated the activities against
Unit 2 polar crane PMT following cable replacement.  
      TSs, the FSAR, 10 CFR Part 50 requirements, licensee procedures, and various
These activities were selected based upon the structure, system, or component's ability  
      NRC generic communications to ensure that the test results adequately ensured that the
to impact risk. The inspectors evaluated these activities for the following (as applicable):  
      equipment met the licensing basis and design requirements. In addition, the inspectors
the effect of testing on the plant had been adequately addressed; testing was adequate  
      reviewed corrective action documents associated with post-maintenance tests to
for the maintenance performed; acceptance criteria were clear and demonstrated  
      determine whether the licensee was identifying problems and entering them in the CAP
operational readiness; test instrumentation was appropriate; tests were performed as  
      and that the problems were being corrected commensurate with their importance to
written in accordance with properly reviewed and approved procedures; equipment was  
      safety. Documents reviewed are listed in the Attachment to this report.
returned to its operational status following testing (temporary modifications or jumpers  
      This inspection constituted four post-maintenance testing samples as defined in
required for test performance were properly removed after test completion); and test  
      IP 71111.19-05.
documentation was properly evaluated. The inspectors evaluated the activities against  
  b. Findings
TSs, the FSAR, 10 CFR Part 50 requirements, licensee procedures, and various  
      No findings of significance were identified.
NRC generic communications to ensure that the test results adequately ensured that the  
                                                25                                      Enclosure
equipment met the licensing basis and design requirements. In addition, the inspectors  
reviewed corrective action documents associated with post-maintenance tests to  
determine whether the licensee was identifying problems and entering them in the CAP  
and that the problems were being corrected commensurate with their importance to  
safety. Documents reviewed are listed in the Attachment to this report.  
This inspection constituted four post-maintenance testing samples as defined in  
IP 71111.19-05.  
b.  
Findings  
No findings of significance were identified.  


1R20 Outage Activities (71111.20)
.1   Refueling Outage Activities
Enclosure
  a. Inspection Scope
26
      The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 2
1R20 Outage Activities (71111.20)  
      RFO, conducted October 15 - December 5, 2009, to confirm that the licensee had
.1  
      appropriately considered risk, industry experience, and previous site-specific problems in
Refueling Outage Activities  
      developing and implementing a plan that assured maintenance of defense-in-depth.
a.  
      During the RFO, the inspectors observed portions of the shutdown and cooldown
Inspection Scope  
      processes and monitored licensee controls over the outage activities listed below.
The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 2  
      Documents reviewed are listed in the Attachment to this report.
RFO, conducted October 15 - December 5, 2009, to confirm that the licensee had  
      *       Licensee configuration management, including maintenance of defense-in-depth
appropriately considered risk, industry experience, and previous site-specific problems in  
              commensurate with the Outage Safety Plan for key safety functions and
developing and implementing a plan that assured maintenance of defense-in-depth.
              compliance with the applicable TS when taking equipment out-of-service.
During the RFO, the inspectors observed portions of the shutdown and cooldown  
      *       Implementation of clearance activities and confirmation that tags were properly
processes and monitored licensee controls over the outage activities listed below.
              hung and equipment appropriately configured to safely support the work or
Documents reviewed are listed in the Attachment to this report.  
              testing.
*  
      *       Installation and configuration of reactor coolant pressure, level, and temperature
Licensee configuration management, including maintenance of defense-in-depth  
              instruments to provide accurate indication, accounting for instrument error.
commensurate with the Outage Safety Plan for key safety functions and  
      *       Controls over the status and configuration of electrical systems to ensure that
compliance with the applicable TS when taking equipment out-of-service.  
              TS and Outage Safety Plan requirements were met, and controls over switchyard
*  
              activities.
Implementation of clearance activities and confirmation that tags were properly  
      *       Monitoring of decay heat removal processes, systems, and components.
hung and equipment appropriately configured to safely support the work or  
      *       Controls to ensure that outage work was not impacting the ability of the operators
testing.  
              to operate the spent fuel pool cooling system.
*  
      *       Reactor water inventory controls, including flow paths, configurations, and
Installation and configuration of reactor coolant pressure, level, and temperature  
              alternative means for inventory addition, and controls to prevent inventory loss.
instruments to provide accurate indication, accounting for instrument error.  
      *       Controls over activities that could affect reactivity.
*  
      *       Maintenance of secondary containment as required by TS.
Controls over the status and configuration of electrical systems to ensure that  
      *       Refueling activities, including fuel handling and activities to detect fuel assembly
TS and Outage Safety Plan requirements were met, and controls over switchyard  
              leakage.
activities.  
      *       Startup and ascension to full power operation, tracking of startup prerequisites,
*  
              walkdown of containment to verify that debris had not been left which could block
Monitoring of decay heat removal processes, systems, and components.  
              emergency core cooling system suction strainers, and reactor physics testing.
*  
      *       Licensee identification and resolution of problems related to RFO activities.
Controls to ensure that outage work was not impacting the ability of the operators  
      This inspection constituted one refueling outage sample as defined in IP 71111.20-05.
to operate the spent fuel pool cooling system.  
  b. Findings
*  
      Momentary Loss of Unit 2 Reactor Vessel Level Indication in the Control Room
Reactor water inventory controls, including flow paths, configurations, and  
      Introduction: A finding of very low safety significance and associated Green NCV of
alternative means for inventory addition, and controls to prevent inventory loss.  
      10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," was
*  
      self-revealed when the licensee performed an Instrumentation and Control (I&C)
Controls over activities that could affect reactivity.  
      procedure that was inappropriate to the circumstances and caused the momentary loss
*  
      of all available channels of reactor vessel level indication in the control room.
Maintenance of secondary containment as required by TS.  
                                                26                                        Enclosure
*  
Refueling activities, including fuel handling and activities to detect fuel assembly  
leakage.  
*  
Startup and ascension to full power operation, tracking of startup prerequisites,  
walkdown of containment to verify that debris had not been left which could block  
emergency core cooling system suction strainers, and reactor physics testing.  
*  
Licensee identification and resolution of problems related to RFO activities.  
This inspection constituted one refueling outage sample as defined in IP 71111.20-05.  
b.  
Findings  
Momentary Loss of Unit 2 Reactor Vessel Level Indication in the Control Room  
Introduction: A finding of very low safety significance and associated Green NCV of  
10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," was  
self-revealed when the licensee performed an Instrumentation and Control (I&C)  
procedure that was inappropriate to the circumstances and caused the momentary loss  
of all available channels of reactor vessel level indication in the control room.  


Description: On October 19, 2009, operators were maintaining reactor vessel inventory
at 70 percent in preparation for head disassembly and placed the reduced inventory
Enclosure
reactor vessel level transmitters (LT), LT-447 and LT-447A, into service for level
27
indication. Subsequently, the operators authorized maintenance to perform
Description: On October 19, 2009, operators were maintaining reactor vessel inventory  
I&C procedure 2ICP 04.023-1, "Reactor Vessel Level Outage Calibration." The purpose
at 70 percent in preparation for head disassembly and placed the reduced inventory  
of the procedure was to calibrate reactor vessel wide and narrow range level
reactor vessel level transmitters (LT), LT-447 and LT-447A, into service for level  
transmitters, 2LT-494, 2LT-495, 2LT-496, and 2LT-497.
indication. Subsequently, the operators authorized maintenance to perform  
During the performance of this procedure, following calibration of 2LT-494, the
I&C procedure 2ICP 04.023-1, "Reactor Vessel Level Outage Calibration." The purpose  
technician valved in the transmitter. This allowed a flow path to exist between the
of the procedure was to calibrate reactor vessel wide and narrow range level  
variable and common reference legs of all the reactor vessel level indicators, which
transmitters, 2LT-494, 2LT-495, 2LT-496, and 2LT-497.  
caused a perturbation on the level indication for 2LT-447 and 2LT-447A, and
During the performance of this procedure, following calibration of 2LT-494, the  
subsequent momentary loss of reactor vessel level indication in the control room.
technician valved in the transmitter. This allowed a flow path to exist between the  
The operators took immediate action to suspend the performance of the I&C procedure
variable and common reference legs of all the reactor vessel level indicators, which  
and sent an operator into containment to verify reactor vessel level via the local
caused a perturbation on the level indication for 2LT-447 and 2LT-447A, and  
standpipe level indicator (LI), LI-447B, and to ensure level indication was reestablished.
subsequent momentary loss of reactor vessel level indication in the control room.
The I&C procedure contained instructions to notify the control operator that perturbations
The operators took immediate action to suspend the performance of the I&C procedure  
on the reactor vessel level indicators 2LT-447 and 2LT-447A may occur and required
and sent an operator into containment to verify reactor vessel level via the local  
operators to verify reduced inventory conditions were not in effect. However, the
standpipe level indicator (LI), LI-447B, and to ensure level indication was reestablished.  
procedure did not contain cautions or prerequisite conditions for the given conditions of
The I&C procedure contained instructions to notify the control operator that perturbations  
being at 70 percent inventory and time-to-boil (TTB) of 17 minutes, essentially the same
on the reactor vessel level indicators 2LT-447 and 2LT-447A may occur and required  
TTB as a reduced inventory condition. No additional barriers were in place to prevent
operators to verify reduced inventory conditions were not in effect. However, the  
the procedure from being performed at the same time as preparations for head
procedure did not contain cautions or prerequisite conditions for the given conditions of  
disassembly.
being at 70 percent inventory and time-to-boil (TTB) of 17 minutes, essentially the same  
Analysis: A performance deficiency was identified when the licensee performed an
TTB as a reduced inventory condition. No additional barriers were in place to prevent  
I&C procedure that was inappropriate for the circumstances of reactor vessel level at
the procedure from being performed at the same time as preparations for head  
70 percent and a TTB of 17 minutes; thereby, causing a loss of all available channels of
disassembly.  
reactor vessel level indication in the control room. The finding was more than minor
Analysis: A performance deficiency was identified when the licensee performed an  
because it is associated with the Mitigating Systems Cornerstone attribute of procedure
I&C procedure that was inappropriate for the circumstances of reactor vessel level at  
quality and adversely affected the associated cornerstone objective to ensure the
70 percent and a TTB of 17 minutes; thereby, causing a loss of all available channels of  
availability, reliability, and capability of systems that respond to initiating events to
reactor vessel level indication in the control room. The finding was more than minor  
prevent undesirable consequences.
because it is associated with the Mitigating Systems Cornerstone attribute of procedure  
In accordance with NRC IMC 0609, Appendix G, "Shutdown Operations Significance
quality and adversely affected the associated cornerstone objective to ensure the  
Determination Process," Attachment 1, Checklist 3, dated May 25, 2004, the inspectors
availability, reliability, and capability of systems that respond to initiating events to  
conducted a Phase 1 SDP screening and determined that the finding required a Phase 2
prevent undesirable consequences.  
analysis since the finding increased the likelihood of a loss of RCS inventory based on
In accordance with NRC IMC 0609, Appendix G, "Shutdown Operations Significance  
loss of reactor vessel level indication in the control room (Sections II(A)(2) II(B)(3) of
Determination Process," Attachment 1, Checklist 3, dated May 25, 2004, the inspectors  
Checklist 3).
conducted a Phase 1 SDP screening and determined that the finding required a Phase 2  
A Region III senior reactor analyst (SRA) performed the assessment using Appendix G,
analysis since the finding increased the likelihood of a loss of RCS inventory based on  
Attachment 2, "Phase 2 Significance Determination Process Template for PWR During
loss of reactor vessel level indication in the control room (Sections II(A)(2) II(B)(3) of  
Shutdown," dated February 28, 2005. The SRA determined this to be a precursor to an
Checklist 3).  
initiating event (a loss of level control precursor - LOLC). The plant operating state
A Region III senior reactor analyst (SRA) performed the assessment using Appendix G,  
(POS) was determined to be "POS 1" (vessel head on and RCS closed). The initiating
Attachment 2, "Phase 2 Significance Determination Process Template for PWR During  
event likelihood for LOLC using Table 1, "Initiating Event Likelihood (IELs) for LOLC
Shutdown," dated February 28, 2005. The SRA determined this to be a precursor to an  
Precursors" was "1," since the time to RHR loss was greater than two hours and action
initiating event (a loss of level control precursor - LOLC). The plant operating state  
to recover RHR could be identified and performed within half of the time to RHR loss.
(POS) was determined to be "POS 1" (vessel head on and RCS closed). The initiating  
The SRA considered this to be an overly conservative value considering that there was
event likelihood for LOLC using Table 1, "Initiating Event Likelihood (IELs) for LOLC  
                                              27                                      Enclosure
Precursors" was "1," since the time to RHR loss was greater than two hours and action  
to recover RHR could be identified and performed within half of the time to RHR loss.
The SRA considered this to be an overly conservative value considering that there was  


no actual loss of RCS inventory, only momentary loss of indication. To better estimate
the IEL, the SRA performed an analysis using the SPAR-H Human Reliability Analysis
Enclosure
Method, NUREG/CR-6883, September 2004.
28
For diagnosis of potential loss of level control, the analyst assumed available time to be
no actual loss of RCS inventory, only momentary loss of indication. To better estimate  
expansive. For action, the analyst assumed stress to be high. All other performance
the IEL, the SRA performed an analysis using the SPAR-H Human Reliability Analysis  
shaping factors were assumed to be nominal. The resultant value of 3E-3 was assumed
Method, NUREG/CR-6883, September 2004.  
as the initiating event likelihood.
For diagnosis of potential loss of level control, the analyst assumed available time to be  
Using Appendix G, Attachment 2, Worksheet 1, "SDP for a PWR Plant - Loss Level
expansive. For action, the analyst assumed stress to be high. All other performance  
Control in POS 1 (RCS Closed)," the SRA evaluated the remaining mitigating capability
shaping factors were assumed to be nominal. The resultant value of 3E-3 was assumed  
credit to reflect equipment availability and the time available to complete tasks prior to
as the initiating event likelihood.  
core damage. The most significant core damage sequences involved loss of steam
Using Appendix G, Attachment 2, Worksheet 1, "SDP for a PWR Plant - Loss Level  
generator cooling and failure of RCS injection and bleed before core damage. The
Control in POS 1 (RCS Closed)," the SRA evaluated the remaining mitigating capability  
combined sequences had a risk significance of about 3E-8. Therefore, the SRA
credit to reflect equipment availability and the time available to complete tasks prior to  
determined that this issue is best characterized as a finding of very low safety
core damage. The most significant core damage sequences involved loss of steam  
significance (Green).
generator cooling and failure of RCS injection and bleed before core damage. The  
The finding had a cross-cutting aspect in the area of human performance, work control
combined sequences had a risk significance of about 3E-8. Therefore, the SRA  
aspect, in that the licensee did not appropriately coordinate work activities for the
determined that this issue is best characterized as a finding of very low safety  
existing plant conditions to ensure the operational impact on reactor vessel level
significance (Green).  
indication while at a water level near reduced inventory (H.3(b)).
The finding had a cross-cutting aspect in the area of human performance, work control  
Enforcement: Title 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and
aspect, in that the licensee did not appropriately coordinate work activities for the  
Drawings," requires, in part, that activities affecting quality be prescribed by documented
existing plant conditions to ensure the operational impact on reactor vessel level  
instructions, procedures, or drawings, of a type appropriate to the circumstances and be
indication while at a water level near reduced inventory (H.3(b)).  
accomplished in accordance with these instructions, procedures or drawings. Contrary
Enforcement: Title 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and  
to this, the licensee performed an I&C procedure that was inappropriate to the
Drawings," requires, in part, that activities affecting quality be prescribed by documented  
circumstances. Specifically, I&C procedure 2ICP 04.023-1, disabled all control room
instructions, procedures, or drawings, of a type appropriate to the circumstances and be  
reactor vessel level indication while the reactor coolant system was at 70 percent reactor
accomplished in accordance with these instructions, procedures or drawings. Contrary  
vessel level. As a result, the indication of reactor water level in the reduced inventory
to this, the licensee performed an I&C procedure that was inappropriate to the  
range was momentarily lost in the control room, which was not appropriate for the
circumstances. Specifically, I&C procedure 2ICP 04.023-1, disabled all control room  
current plant condition. Because this violation was of very low safety significance and it
reactor vessel level indication while the reactor coolant system was at 70 percent reactor  
was entered into the licensee's CAP (AR 01158914), this violation is being treated as an
vessel level. As a result, the indication of reactor water level in the reduced inventory  
NCV consistent with section VI.A.1. of the NRC Enforcement Policy
range was momentarily lost in the control room, which was not appropriate for the  
(NCV 05000301/2009005-05).
current plant condition. Because this violation was of very low safety significance and it  
The licensee took immediate action to suspend the performance of the I&C procedure
was entered into the licensee's CAP (AR 01158914), this violation is being treated as an  
and sent an operator into containment to verify reactor vessel level via the local
NCV consistent with section VI.A.1. of the NRC Enforcement Policy  
standpipe level indicator (LI-447B) to ensure level indication was reestablished.
(NCV 05000301/2009005-05).  
Additionally, the licensee has applied work planning logic to this activity to ensure the
The licensee took immediate action to suspend the performance of the I&C procedure  
reactor is defueled prior to beginning the calibration and is evaluating necessary
and sent an operator into containment to verify reactor vessel level via the local  
revisions to the I&C procedure.
standpipe level indicator (LI-447B) to ensure level indication was reestablished.
                                          28                                      Enclosure
Additionally, the licensee has applied work planning logic to this activity to ensure the  
reactor is defueled prior to beginning the calibration and is evaluating necessary  
revisions to the I&C procedure.  


1R22 Surveillance Testing (71111.22)
.1   Surveillance Testing
Enclosure
  a. Inspection Scope
29
      The inspectors reviewed the test results for the following activities to determine whether
1R22 Surveillance Testing (71111.22)  
      risk-significant systems and equipment were capable of performing their intended safety
.1  
      function and to verify testing was conducted in accordance with applicable procedural
Surveillance Testing  
      and TS requirements:
a.  
      *       Unit 2 ORT 3A/B EDG loss of offsite power loss of coolant accident routine test;
Inspection Scope  
      *       OSHA [Occupational Safety and Health Administration] polar crane inspection;
The inspectors reviewed the test results for the following activities to determine whether  
              and
risk-significant systems and equipment were capable of performing their intended safety  
      *       Unit 2 turbine-driven AFW pump and valve inservice test.
function and to verify testing was conducted in accordance with applicable procedural  
      The inspectors observed in-plant activities and reviewed procedures and associated
and TS requirements:  
      records to determine the following:
*  
      *       did preconditioning occur;
Unit 2 ORT 3A/B EDG loss of offsite power loss of coolant accident routine test;  
      *       were the effects of the testing adequately addressed by control room personnel
*  
              or engineers prior to the commencement of the testing;
OSHA [Occupational Safety and Health Administration] polar crane inspection;  
      *       were acceptance criteria clearly stated, demonstrated operational readiness, and
and  
              consistent with the system design basis;
*  
      *       plant equipment calibration was correct, accurate, and properly documented;
Unit 2 turbine-driven AFW pump and valve inservice test.  
      *       as-left setpoints were within required ranges; and the calibration frequency were
The inspectors observed in-plant activities and reviewed procedures and associated  
              in accordance with TSs, the USAR, procedures, and applicable commitments;
records to determine the following:  
      *       measuring and test equipment calibration was current;
*  
      *       test equipment was used within the required range and accuracy; applicable
did preconditioning occur;
              prerequisites described in the test procedures were satisfied;
*  
      *       test frequencies met TS requirements to demonstrate operability and reliability;
were the effects of the testing adequately addressed by control room personnel  
              tests were performed in accordance with the test procedures and other
or engineers prior to the commencement of the testing;  
              applicable procedures; jumpers and lifted leads were controlled and restored
*  
              where used;
were acceptance criteria clearly stated, demonstrated operational readiness, and  
      *       test data and results were accurate, complete, within limits, and valid;
consistent with the system design basis;  
      *       test equipment was removed after testing;
*  
      *       where applicable for inservice testing activities, testing was performed in
plant equipment calibration was correct, accurate, and properly documented;  
              accordance with the applicable version of ASME Code Section XI, and reference
*  
              values were consistent with the system design basis;
as-left setpoints were within required ranges; and the calibration frequency were  
      *       where applicable, test results not meeting acceptance criteria were addressed
in accordance with TSs, the USAR, procedures, and applicable commitments;  
              with an adequate operability evaluation or the system or component was
*  
              declared inoperable;
measuring and test equipment calibration was current;  
      *       where applicable for safety-related instrument control surveillance tests,
*  
              reference setting data were accurately incorporated in the test procedure;
test equipment was used within the required range and accuracy; applicable  
      *       where applicable, actual conditions encountering high resistance electrical
prerequisites described in the test procedures were satisfied;  
              contacts were such that the intended safety function could still be accomplished;
*  
      *       prior procedure changes had not provided an opportunity to identify problems
test frequencies met TS requirements to demonstrate operability and reliability;  
              encountered during the performance of the surveillance or calibration test;
tests were performed in accordance with the test procedures and other  
                                              29                                      Enclosure
applicable procedures; jumpers and lifted leads were controlled and restored  
where used;  
*  
test data and results were accurate, complete, within limits, and valid;  
*  
test equipment was removed after testing;  
*  
where applicable for inservice testing activities, testing was performed in  
accordance with the applicable version of ASME Code Section XI, and reference  
values were consistent with the system design basis;  
*  
where applicable, test results not meeting acceptance criteria were addressed  
with an adequate operability evaluation or the system or component was  
declared inoperable;  
*  
where applicable for safety-related instrument control surveillance tests,  
reference setting data were accurately incorporated in the test procedure;  
*  
where applicable, actual conditions encountering high resistance electrical  
contacts were such that the intended safety function could still be accomplished;  
*  
prior procedure changes had not provided an opportunity to identify problems  
encountered during the performance of the surveillance or calibration test;  


      *       equipment was returned to a position or status required to support the
              performance of its safety functions; and
Enclosure
      *       all problems identified during the testing were appropriately documented and
30
              dispositioned in the CAP.
*  
      Documents reviewed are listed in the Attachment to this report.
equipment was returned to a position or status required to support the  
      This inspection constituted two routine surveillance testing samples and one inservice
performance of its safety functions; and  
      testing sample as defined in IP 71111.22, Sections -02 and -05.
*  
  b. Findings
all problems identified during the testing were appropriately documented and  
      No findings of significance were identified.
dispositioned in the CAP.  
      Cornerstone: Emergency Preparedness
Documents reviewed are listed in the Attachment to this report.  
1EP2 Alert and Notification System (ANS) Evaluation (71114.02)
This inspection constituted two routine surveillance testing samples and one inservice  
.1   ANS Evaluation
testing sample as defined in IP 71111.22, Sections -02 and -05.  
  a. Inspection Scope
b.  
      The inspectors reviewed documents and conducted discussions with Emergency
Findings  
      Preparedness (EP) staff and management regarding the operation, maintenance, and
No findings of significance were identified.  
      periodic testing of the ANS in the Point Beach Plant's plume pathway Emergency
Cornerstone: Emergency Preparedness  
      Planning Zone. The inspectors reviewed monthly trend reports and the daily and
1EP2 Alert and Notification System (ANS) Evaluation (71114.02)  
      monthly operability records from October 2007 through November 2009. Information
.1  
      gathered during document reviews and interviews was used to determine whether the
ANS Evaluation  
      ANS equipment was maintained and tested in accordance with Emergency Plan
a.  
      commitments and procedures. Documents reviewed are listed in the Attachment to this
Inspection Scope  
      report.
The inspectors reviewed documents and conducted discussions with Emergency  
      This alert and notification system inspection constituted one sample as defined in
Preparedness (EP) staff and management regarding the operation, maintenance, and  
      IP 71114.02-05.
periodic testing of the ANS in the Point Beach Plant's plume pathway Emergency  
  b. Findings
Planning Zone. The inspectors reviewed monthly trend reports and the daily and  
      No findings of significance were identified.
monthly operability records from October 2007 through November 2009. Information  
1EP3 Emergency Response Organization (ERO) Augmentation Testing (71114.03)
gathered during document reviews and interviews was used to determine whether the  
.1   ERO Augmentation Testing
ANS equipment was maintained and tested in accordance with Emergency Plan  
  a. Inspection Scope
commitments and procedures. Documents reviewed are listed in the Attachment to this  
      The inspectors reviewed and discussed with plant EP management and staff the
report.  
      emergency plan commitments and procedures that addressed the primary and alternate
This alert and notification system inspection constituted one sample as defined in  
      methods of initiating an ERO activation to augment the on-shift ERO as well as the
IP 71114.02-05.  
      provisions for maintaining the station's ERO qualification and team lists. The inspectors
b.  
      reviewed reports and a sample of CAP records of unannounced off-hour augmentation
Findings  
      tests and pager test, which were conducted between March 2008 and September 2009,
No findings of significance were identified.  
                                                30                                    Enclosure
1EP3 Emergency Response Organization (ERO) Augmentation Testing (71114.03)  
.1  
ERO Augmentation Testing  
a.  
Inspection Scope  
The inspectors reviewed and discussed with plant EP management and staff the  
emergency plan commitments and procedures that addressed the primary and alternate  
methods of initiating an ERO activation to augment the on-shift ERO as well as the  
provisions for maintaining the station's ERO qualification and team lists. The inspectors  
reviewed reports and a sample of CAP records of unannounced off-hour augmentation  
tests and pager test, which were conducted between March 2008 and September 2009,  


      to determine the adequacy of the drill critiques and associated corrective actions. The
      inspectors also reviewed a sample of the EP training records of approximately
Enclosure
      37 ERO personnel, who were assigned to key and support positions, to determine the
31
      status of their training as it related to their assigned ERO positions. Documents
to determine the adequacy of the drill critiques and associated corrective actions. The  
      reviewed are listed in the Attachment to this report.
inspectors also reviewed a sample of the EP training records of approximately  
      This emergency response organization augmentation testing inspection constituted one
37 ERO personnel, who were assigned to key and support positions, to determine the  
      sample as defined in IP 71114.03-05.
status of their training as it related to their assigned ERO positions. Documents  
  b. Findings
reviewed are listed in the Attachment to this report.  
      No findings of significance were identified.
This emergency response organization augmentation testing inspection constituted one  
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
sample as defined in IP 71114.03-05.  
.1   Emergency Action Level and Emergency Plan Changes
b.  
  a. Inspection Scope
Findings  
      Since the last NRC inspection of this program area, emergency action level and
No findings of significance were identified.  
      Emergency Plan revisions were implemented based on the licensees determination, in
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)  
      accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in
.1  
      effectiveness of the Plan, and that the revised Plan as changed continues to meet the
Emergency Action Level and Emergency Plan Changes  
      requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. Revisions to the
a.  
      emergency action levels and emergency plan reviewed by the inspectors included:
Inspection Scope  
      1) EP 2.0, Revision 46; 2) EP 6.0, Revisions 51 and 52; 3) Appendix M, Revision 2; and
Since the last NRC inspection of this program area, emergency action level and  
      4) EPIP 1.2.1, Revision 3. The inspectors conducted a sampling review of the
Emergency Plan revisions were implemented based on the licensees determination, in  
      Emergency Plan changes and a review of the Emergency Action Level changes to
accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in  
      evaluate for potential decreases in effectiveness of the Plan. However, this review does
effectiveness of the Plan, and that the revised Plan as changed continues to meet the  
      not constitute formal NRC approval of the changes. Therefore, these changes remain
requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. Revisions to the  
      subject to future NRC inspection in their entirety.
emergency action levels and emergency plan reviewed by the inspectors included:
      This emergency action level and emergency plan changes inspection constituted one
1) EP 2.0, Revision 46; 2) EP 6.0, Revisions 51 and 52; 3) Appendix M, Revision 2; and  
      sample as defined in IP 71114.04-05.
4) EPIP 1.2.1, Revision 3. The inspectors conducted a sampling review of the  
  b. Findings
Emergency Plan changes and a review of the Emergency Action Level changes to  
      No findings of significance were identified.
evaluate for potential decreases in effectiveness of the Plan. However, this review does  
1EP5 Correction of EP Weaknesses and Deficiencies (71114.05)
not constitute formal NRC approval of the changes. Therefore, these changes remain  
.1   Correction of EP Weaknesses and Deficiencies
subject to future NRC inspection in their entirety.  
  a. Inspection Scope
This emergency action level and emergency plan changes inspection constituted one  
      The inspectors reviewed a sample of Nuclear Oversight 2008 and 2009 audits of the
sample as defined in IP 71114.04-05.  
      Point Beach EP program to determine that the independent assessments met the
b.  
      requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports and
Findings  
      samples of CAP records associated with the 2008 biennial exercise, as well as various
No findings of significance were identified.  
      EP drills conducted in 2007, 2008, and 2009, in order to determine whether the licensee
1EP5 Correction of EP Weaknesses and Deficiencies (71114.05)  
      fulfilled drill commitments and to evaluate the licensee's efforts to identify and resolve
.1  
                                                  31                                      Enclosure
Correction of EP Weaknesses and Deficiencies  
a.  
Inspection Scope  
The inspectors reviewed a sample of Nuclear Oversight 2008 and 2009 audits of the  
Point Beach EP program to determine that the independent assessments met the  
requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports and  
samples of CAP records associated with the 2008 biennial exercise, as well as various  
EP drills conducted in 2007, 2008, and 2009, in order to determine whether the licensee  
fulfilled drill commitments and to evaluate the licensee's efforts to identify and resolve  


      identified issues. The inspectors reviewed a sample of EP items and corrective actions
      related to the facility's EP program and activities to determine whether corrective actions
Enclosure
      were completed in accordance with the site's CAP. Documents reviewed are listed in
32
      the Attachment to this report.
identified issues. The inspectors reviewed a sample of EP items and corrective actions  
      This correction of emergency preparedness weaknesses and deficiencies inspection
related to the facility's EP program and activities to determine whether corrective actions  
      constituted one sample as defined in IP 71114.05-05.
were completed in accordance with the site's CAP. Documents reviewed are listed in  
  b. Findings
the Attachment to this report.  
      No findings of significance were identified.
This correction of emergency preparedness weaknesses and deficiencies inspection  
2.   RADIATION SAFETY
constituted one sample as defined in IP 71114.05-05.  
      Cornerstone: Occupational Radiation Safety
b.  
2OS1 Access Control to Radiologically Significant Areas (71121.01)
Findings  
.1   Review of Licensee Performance Indicators (PIs) for the Occupational Exposure
No findings of significance were identified.  
      Cornerstone
2.  
  a. Inspection Scope
RADIATION SAFETY  
      The inspectors reviewed the licensee's Occupational Exposure Control Cornerstone PI
Cornerstone: Occupational Radiation Safety  
      to determine whether the conditions resulting in any PI occurrences had been evaluated
2OS1 Access Control to Radiologically Significant Areas (71121.01)  
      and whether identified problems had been entered into the licensee's CAP for resolution.
.1  
      This inspection constituted one sample as defined in IP 71121.01-5.
Review of Licensee Performance Indicators (PIs) for the Occupational Exposure  
  b. Findings
Cornerstone  
      No findings of significance were identified.
a.  
.2   Plant Walkdowns and Radiation Work Permit (RWP) Reviews
Inspection Scope  
  a. Inspection Scope
The inspectors reviewed the licensee's Occupational Exposure Control Cornerstone PI  
      The inspectors reviewed licensee controls and surveys in the following radiologically
to determine whether the conditions resulting in any PI occurrences had been evaluated  
      significant work areas within radiation areas, high radiation areas, and airborne
and whether identified problems had been entered into the licensee's CAP for resolution.  
      radioactivity areas in the plant to determine if radiological controls including surveys,
This inspection constituted one sample as defined in IP 71121.01-5.  
      postings, and barricades were acceptable:
b.  
      *       Auxiliary Building;
Findings  
      *       Containment Building;
No findings of significance were identified.  
      *       Spent Fuel Pool.
.2  
      This inspection constituted one sample as defined in IP 71121.01-5.
Plant Walkdowns and Radiation Work Permit (RWP) Reviews  
      The inspectors reviewed the RWPs and work packages used to access these areas and
a.  
      other high radiation work areas. The inspectors assessed the work control instructions
Inspection Scope  
      and control barriers specified by the licensee. Electronic dosimeter alarm setpoints for
The inspectors reviewed licensee controls and surveys in the following radiologically  
                                                32                                        Enclosure
significant work areas within radiation areas, high radiation areas, and airborne  
radioactivity areas in the plant to determine if radiological controls including surveys,  
postings, and barricades were acceptable:  
*  
Auxiliary Building;  
*  
Containment Building;  
*  
Spent Fuel Pool.  
This inspection constituted one sample as defined in IP 71121.01-5.  
The inspectors reviewed the RWPs and work packages used to access these areas and  
other high radiation work areas. The inspectors assessed the work control instructions  
and control barriers specified by the licensee. Electronic dosimeter alarm setpoints for  


    both integrated dose and dose rate were evaluated for conformity with survey indications
    and plant policy. The inspectors interviewed workers to verify that they were aware of
Enclosure
    the actions required if their electronic dosimeters noticeably malfunctioned or alarmed.
33
    This inspection constituted one sample as defined in IP 71121.01-5.
both integrated dose and dose rate were evaluated for conformity with survey indications  
    The inspectors walked down and surveyed (using an NRC survey meter) these areas to
and plant policy. The inspectors interviewed workers to verify that they were aware of  
    verify that the prescribed RWP, procedure, and engineering controls were in place; that
the actions required if their electronic dosimeters noticeably malfunctioned or alarmed.  
    licensee surveys and postings were complete and accurate; and that air samplers were
This inspection constituted one sample as defined in IP 71121.01-5.  
    properly located.
The inspectors walked down and surveyed (using an NRC survey meter) these areas to  
    This inspection constituted one sample as defined in IP 71121.01-5.
verify that the prescribed RWP, procedure, and engineering controls were in place; that  
    The inspectors reviewed RWPs for airborne radioactivity areas to verify barrier integrity
licensee surveys and postings were complete and accurate; and that air samplers were  
    and engineering controls performance (e.g., high-efficiency particulate air ventilation
properly located.  
    system operation) and to determine if there was a potential for individual worker internal
This inspection constituted one sample as defined in IP 71121.01-5.  
    exposures in excess of 50 millirem committed effective dose equivalent (EDE). There
The inspectors reviewed RWPs for airborne radioactivity areas to verify barrier integrity  
    were no airborne radioactivity work areas during the inspection period.
and engineering controls performance (e.g., high-efficiency particulate air ventilation  
    Work areas having a history of, or the potential for, airborne transuranics were evaluated
system operation) and to determine if there was a potential for individual worker internal  
    to verify that the licensee had considered the potential for transuranic isotopes and had
exposures in excess of 50 millirem committed effective dose equivalent (EDE). There  
    provided appropriate worker protection.
were no airborne radioactivity work areas during the inspection period.  
    This inspection constituted one sample as defined in IP 71121.01-5.
Work areas having a history of, or the potential for, airborne transuranics were evaluated  
    The inspectors assessed the adequacy of the licensee's internal dose assessment
to verify that the licensee had considered the potential for transuranic isotopes and had  
    process for internal exposures in excess of 50 millirem committed EDE. There were no
provided appropriate worker protection.  
    internal exposures greater than 50 millirem committed EDE.
This inspection constituted one sample as defined in IP 71121.01-5.  
    This inspection constituted one sample as defined in IP 71121.01-5.
The inspectors assessed the adequacy of the licensee's internal dose assessment  
    The inspectors also reviewed the licensee's physical and programmatic controls for
process for internal exposures in excess of 50 millirem committed EDE. There were no  
    highly activated and/or contaminated materials (non-fuel) stored within the spent fuel
internal exposures greater than 50 millirem committed EDE.  
    pool or other storage pools.
This inspection constituted one sample as defined in IP 71121.01-5.  
    This inspection constituted one sample as defined in IP 71121.01-5.
The inspectors also reviewed the licensee's physical and programmatic controls for  
  b. Findings
highly activated and/or contaminated materials (non-fuel) stored within the spent fuel  
    No findings of significance were identified.
pool or other storage pools.  
.3   Problem Identification and Resolution
This inspection constituted one sample as defined in IP 71121.01-5.  
  a. Inspection Scope
b.  
    The inspectors reviewed a sample of the licensee's self-assessments, audits, Licensee
Findings  
    Event Reports (LERs), and Special Reports related to the access control program to
No findings of significance were identified.  
    verify that identified problems were entered into the CAP for resolution.
.3  
    This inspection constituted one sample as defined in IP 71121.01-5.
Problem Identification and Resolution  
                                              33                                      Enclosure
a.  
Inspection Scope  
The inspectors reviewed a sample of the licensee's self-assessments, audits, Licensee  
Event Reports (LERs), and Special Reports related to the access control program to  
verify that identified problems were entered into the CAP for resolution.  
This inspection constituted one sample as defined in IP 71121.01-5.  


    The inspectors reviewed corrective action reports related to access controls and any
    high radiation area radiological incidents (issues that did not count as PI occurrences
Enclosure
    identified by the licensee in high radiation areas less than 1R/hr). Staff members were
34
    interviewed and corrective action documents were reviewed to verify that follow-up
The inspectors reviewed corrective action reports related to access controls and any  
    activities were being conducted in an effective and timely manner commensurate with
high radiation area radiological incidents (issues that did not count as PI occurrences  
    their importance to safety and risk based on the following:
identified by the licensee in high radiation areas less than 1R/hr). Staff members were  
    *       initial problem identification, characterization, and tracking;
interviewed and corrective action documents were reviewed to verify that follow-up  
    *       disposition of operability/reportability issues;
activities were being conducted in an effective and timely manner commensurate with  
    *       evaluation of safety significance/risk and priority for resolution;
their importance to safety and risk based on the following:  
    *       identification of repetitive problems;
*  
    *       identification of contributing causes;
initial problem identification, characterization, and tracking;  
    *       identification and implementation of effective corrective actions;
*  
    *       resolution of NCVs tracked in the corrective action system; and
disposition of operability/reportability issues;  
    *       implementation/consideration of risk significant operational experience feedback.
*  
    This inspection constituted one sample as defined in IP 71121.01-5.
evaluation of safety significance/risk and priority for resolution;  
    The inspectors evaluated the licensee's process for problem identification,
*  
    characterization, and prioritization and verified that problems were entered into the CAP
identification of repetitive problems;  
    and resolved. For repetitive deficiencies and/or significant individual deficiencies in
*  
    problem identification and resolution, the inspectors verified that the licensee's
identification of contributing causes;  
    self-assessment activities were capable of identifying and addressing these deficiencies.
*  
    This inspection constituted one sample as defined in IP 71121.01-5.
identification and implementation of effective corrective actions;  
    The inspectors reviewed licensee documentation packages for all PI events occurring
*  
    since the last inspection to determine if any of these PI events involved dose rates in
resolution of NCVs tracked in the corrective action system; and  
    excess of 25 R/hr at 30 centimeters or in excess of 500 R/hr at 1 meter. Barriers were
*  
    evaluated for failure and to determine if there were any barriers left to prevent personnel
implementation/consideration of risk significant operational experience feedback.  
    access. Unintended exposures exceeding 100 millirem total EDE (or 5 rem shallow
This inspection constituted one sample as defined in IP 71121.01-5.  
    dose equivalent or 1.5 rem lens dose equivalent) were evaluated to determine if there
The inspectors evaluated the licensee's process for problem identification,  
    were any regulatory overexposures or if there was a substantial potential for an
characterization, and prioritization and verified that problems were entered into the CAP  
    overexposure.
and resolved. For repetitive deficiencies and/or significant individual deficiencies in  
    This inspection constituted one sample as defined in IP 71121.01-5.
problem identification and resolution, the inspectors verified that the licensee's  
  b. Findings
self-assessment activities were capable of identifying and addressing these deficiencies.  
    No findings of significance were identified.
This inspection constituted one sample as defined in IP 71121.01-5.  
.4   Job-In-Progress Reviews
The inspectors reviewed licensee documentation packages for all PI events occurring  
  a. Inspection Scope
since the last inspection to determine if any of these PI events involved dose rates in  
    The inspectors observed the following three jobs that were being performed in radiation
excess of 25 R/hr at 30 centimeters or in excess of 500 R/hr at 1 meter. Barriers were  
    areas, airborne radioactivity areas, or high radiation areas for observation of work
evaluated for failure and to determine if there were any barriers left to prevent personnel  
    activities that presented the greatest radiological risk to workers:
access. Unintended exposures exceeding 100 millirem total EDE (or 5 rem shallow  
                                                34                                    Enclosure
dose equivalent or 1.5 rem lens dose equivalent) were evaluated to determine if there  
were any regulatory overexposures or if there was a substantial potential for an  
overexposure.  
This inspection constituted one sample as defined in IP 71121.01-5.  
b.  
Findings  
No findings of significance were identified.  
.4  
Job-In-Progress Reviews  
a.  
Inspection Scope  
The inspectors observed the following three jobs that were being performed in radiation  
areas, airborne radioactivity areas, or high radiation areas for observation of work  
activities that presented the greatest radiological risk to workers:  


    *       insulation activities;
    *       reactor coolant pump activities; and
Enclosure
    *       core barrel movement activities.
35
    The inspectors reviewed radiological job requirements for these activities, including
*  
    RWP requirements and work procedure requirements, and attended
insulation activities;  
    As-Low-As-Is-Reasonably-Achievable (ALARA) job briefings.
*  
    This inspection constituted one sample as defined in IP 71121.01-5.
reactor coolant pump activities; and  
    Job performance was observed with respect to the radiological control requirements to
*  
    assess whether radiological conditions in the work area were adequately communicated
core barrel movement activities.  
    to workers through pre-job briefings and postings. The inspectors evaluated the
The inspectors reviewed radiological job requirements for these activities, including  
    adequacy of radiological controls, including required radiation, contamination, and
RWP requirements and work procedure requirements, and attended  
    airborne surveys for system breaches; radiation protection job coverage, including any
As-Low-As-Is-Reasonably-Achievable (ALARA) job briefings.
    applicable audio and visual surveillance for remote job coverage; and contamination
This inspection constituted one sample as defined in IP 71121.01-5.  
    controls.
Job performance was observed with respect to the radiological control requirements to  
    This inspection constituted one sample as defined in IP 71121.01-5.
assess whether radiological conditions in the work area were adequately communicated  
    The inspectors reviewed radiological work in high radiation work areas having significant
to workers through pre-job briefings and postings. The inspectors evaluated the  
    dose rate gradients to evaluate whether the licensee adequately monitored exposure to
adequacy of radiological controls, including required radiation, contamination, and  
    personnel and to assess the adequacy of licensee controls. These work areas involved
airborne surveys for system breaches; radiation protection job coverage, including any  
    areas where the dose rate gradients were severe, thereby increasing the necessity of
applicable audio and visual surveillance for remote job coverage; and contamination  
    providing multiple dosimeters or enhanced job controls.
controls.  
    This inspection constituted one sample as defined in IP 71121.01-5.
This inspection constituted one sample as defined in IP 71121.01-5.  
  b. Findings
The inspectors reviewed radiological work in high radiation work areas having significant  
    No findings of significance were identified.
dose rate gradients to evaluate whether the licensee adequately monitored exposure to  
.5   High Risk Significant, High Dose Rate, High Radiation Area, and Very High Radiation
personnel and to assess the adequacy of licensee controls. These work areas involved  
    Area Controls
areas where the dose rate gradients were severe, thereby increasing the necessity of  
  a. Inspection Scope
providing multiple dosimeters or enhanced job controls.  
    The inspectors held discussions with the Radiation Protection Manager concerning high
This inspection constituted one sample as defined in IP 71121.01-5.  
    dose rate, high radiation area, and very high radiation area controls and procedures,
b.  
    including procedural changes that had occurred since the last inspection, in order to
Findings  
    assess whether any procedure modifications substantially reduced the effectiveness and
No findings of significance were identified.  
    level of worker protection.
.5  
    This inspection constituted one sample as defined in IP 71121.01-5.
High Risk Significant, High Dose Rate, High Radiation Area, and Very High Radiation  
    The inspectors discussed with radiation protection supervisors the controls that were in
Area Controls  
    place for special areas of the plant that had the potential to become very high radiation
a.  
    areas during certain plant operations. The inspectors assessed if plant operations
Inspection Scope  
    required communication beforehand with the radiation protection group, so as to allow
The inspectors held discussions with the Radiation Protection Manager concerning high  
    corresponding timely actions to properly post and control the radiation hazards.
dose rate, high radiation area, and very high radiation area controls and procedures,  
                                              35                                    Enclosure
including procedural changes that had occurred since the last inspection, in order to  
assess whether any procedure modifications substantially reduced the effectiveness and  
level of worker protection.  
This inspection constituted one sample as defined in IP 71121.01-5.  
The inspectors discussed with radiation protection supervisors the controls that were in  
place for special areas of the plant that had the potential to become very high radiation  
areas during certain plant operations. The inspectors assessed if plant operations  
required communication beforehand with the radiation protection group, so as to allow  
corresponding timely actions to properly post and control the radiation hazards.  


    This inspection constituted one sample as defined in IP 71121.01-5.
    The inspectors conducted plant walkdowns to assess the posting and locking of
Enclosure
    entrances to high dose rate, high radiation areas, and very high radiation areas.
36
    This inspection constituted one sample as defined in IP 71121.01-5.
This inspection constituted one sample as defined in IP 71121.01-5.  
  b. Findings
The inspectors conducted plant walkdowns to assess the posting and locking of  
    No findings of significance were identified.
entrances to high dose rate, high radiation areas, and very high radiation areas.  
.6   Radiation Worker Performance
This inspection constituted one sample as defined in IP 71121.01-5.  
  a. Inspection Scope
b.  
    During job performance observations, the inspectors evaluated radiation worker
Findings  
    performance with respect to stated radiation safety work requirements. The inspectors
No findings of significance were identified.  
    evaluated whether workers were aware of any significant radiological conditions in their
.6  
    workplace, of the RWP controls and limits in place, and of the level of radiological
Radiation Worker Performance  
    hazards present. The inspectors also observed worker performance to determine if
a.  
    workers accounted for these radiological hazards.
Inspection Scope  
    This inspection constituted one sample as defined in IP 71121.01-5.
During job performance observations, the inspectors evaluated radiation worker  
    The inspectors reviewed radiological problem reports for which the cause of the event
performance with respect to stated radiation safety work requirements. The inspectors  
    was due to radiation worker errors to determine if there was an observable pattern
evaluated whether workers were aware of any significant radiological conditions in their  
    traceable to a similar cause and to determine if this perspective matched the corrective
workplace, of the RWP controls and limits in place, and of the level of radiological  
    action approach taken by the licensee to resolve the reported problems. Problems or
hazards present. The inspectors also observed worker performance to determine if  
    issues with planned or completed corrective actions were discussed with the Radiation
workers accounted for these radiological hazards.  
    Protection Manager.
This inspection constituted one sample as defined in IP 71121.01-5.  
    This inspection constituted one sample as defined in IP 71121.01-5.
The inspectors reviewed radiological problem reports for which the cause of the event  
  b. Findings
was due to radiation worker errors to determine if there was an observable pattern  
    No findings of significance were identified.
traceable to a similar cause and to determine if this perspective matched the corrective  
.7   Radiation Protection Technician Proficiency
action approach taken by the licensee to resolve the reported problems. Problems or  
  a. Inspection Scope
issues with planned or completed corrective actions were discussed with the Radiation  
    During job performance observations, the inspectors evaluated radiation protection
Protection Manager.  
    technician performance with respect to radiation safety work requirements. The
This inspection constituted one sample as defined in IP 71121.01-5.  
    inspectors evaluated whether technicians were aware of the radiological conditions in
b.  
    their workplace, the RWP controls and limits in place, and if their performance was
Findings  
    consistent with their training and qualifications with respect to the radiological hazards
No findings of significance were identified.  
    and work activities.
.7  
    This inspection constituted one sample as defined in IP 71121.01-5.
Radiation Protection Technician Proficiency  
    The inspectors reviewed radiological problem reports for which the cause of the event
a.  
    was radiation protection technician error to determine if there was an observable pattern
Inspection Scope  
                                                36                                      Enclosure
During job performance observations, the inspectors evaluated radiation protection  
technician performance with respect to radiation safety work requirements. The  
inspectors evaluated whether technicians were aware of the radiological conditions in  
their workplace, the RWP controls and limits in place, and if their performance was  
consistent with their training and qualifications with respect to the radiological hazards  
and work activities.  
This inspection constituted one sample as defined in IP 71121.01-5.  
The inspectors reviewed radiological problem reports for which the cause of the event  
was radiation protection technician error to determine if there was an observable pattern  


      traceable to a similar cause and to determine if this perspective matched the corrective
      action approach taken by the licensee to resolve the reported problems.
Enclosure
      This inspection constituted one sample as defined in IP 71121.01-5.
37
  b. Findings
traceable to a similar cause and to determine if this perspective matched the corrective  
      No findings of significance were identified.
action approach taken by the licensee to resolve the reported problems.  
2OS2 ALARA Planning and Controls (71121.02)
This inspection constituted one sample as defined in IP 71121.01-5.  
.1   Radiological Work Planning
b.  
  a. Inspection Scope
Findings  
      The inspectors compared the results achieved (including dose rate reductions and
No findings of significance were identified.  
      person-rem used) with the intended dose established in the licensee's ALARA planning
2OS2 ALARA Planning and Controls (71121.02)  
      for GSI-191 insulation removal activities. Reasons for inconsistencies between intended
.1  
      and actual work activity doses were reviewed.
Radiological Work Planning  
      This inspection constituted one required sample as defined in IP 71121.02-5.
a.  
  b. Findings
Inspection Scope  
      No findings of significance were identified.
The inspectors compared the results achieved (including dose rate reductions and  
.2   Verification of Dose Estimates and Exposure Tracking Systems
person-rem used) with the intended dose established in the licensee's ALARA planning  
  a. Inspection Scope
for GSI-191 insulation removal activities. Reasons for inconsistencies between intended  
      The licensee's process for adjusting exposure estimates or re-planning work (when
and actual work activity doses were reviewed.  
      unexpected changes in scope, emergent work, or higher than anticipated radiation levels
This inspection constituted one required sample as defined in IP 71121.02-5.  
      were encountered) was evaluated. This included determining whether adjustments to
b.  
      estimated exposure (intended dose) were based on sound radiation protection and
Findings  
      ALARA principles or whether they resulted from failures to adequately plan or to control
No findings of significance were identified.  
      the work. The frequency of these adjustments was reviewed to evaluate the adequacy
.2  
      of the original ALARA planning process.
Verification of Dose Estimates and Exposure Tracking Systems  
      This inspection constituted one required sample as defined in IP 71121.02-5.
a.  
  b. Findings
Inspection Scope  
      No findings of significance were identified.
The licensee's process for adjusting exposure estimates or re-planning work (when  
.3   Problem Identification and Resolutions
unexpected changes in scope, emergent work, or higher than anticipated radiation levels  
  a. Inspection Scope
were encountered) was evaluated. This included determining whether adjustments to  
      The inspectors reviewed the licensee's self-assessments, audits, and Special Reports
estimated exposure (intended dose) were based on sound radiation protection and  
      related to the ALARA program since the last inspection to determine if the licensee's
ALARA principles or whether they resulted from failures to adequately plan or to control  
      overall audit program's scope and frequency for all applicable areas under the
the work. The frequency of these adjustments was reviewed to evaluate the adequacy  
      Occupational Radiation Safety Cornerstone met the requirements of 10 CFR 20.1101(c).
of the original ALARA planning process.  
                                              37                                    Enclosure
This inspection constituted one required sample as defined in IP 71121.02-5.  
b.  
Findings  
No findings of significance were identified.  
.3  
Problem Identification and Resolutions  
a.  
Inspection Scope  
The inspectors reviewed the licensee's self-assessments, audits, and Special Reports  
related to the ALARA program since the last inspection to determine if the licensee's  
overall audit program's scope and frequency for all applicable areas under the  
Occupational Radiation Safety Cornerstone met the requirements of 10 CFR 20.1101(c).  


      This inspection constituted one required sample as defined in IP 71121.02-5.
  b. Findings
Enclosure
      No findings of significance were identified.
38
4.   OTHER ACTIVITIES
This inspection constituted one required sample as defined in IP 71121.02-5.  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
b.  
      Preparedness, Public Radiation Safety, and Occupational Radiation Safety
Findings  
4OA1 PI Verification (71151)
No findings of significance were identified.  
.1   Mitigating Systems Performance Index (MSPI) - Heat Removal System
4.  
  a. Inspection Scope
OTHER ACTIVITIES  
      The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
      Unit 1 and Unit 2 for the third quarter 2008 through the second quarter of 2009.
Preparedness, Public Radiation Safety, and Occupational Radiation Safety  
      To determine the accuracy of this PI data, definitions and guidance contained in the
4OA1 PI Verification (71151)  
      Nuclear Energy Initiative (NEI) Document 99-02, "Regulatory Assessment Performance
.1  
      Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's
Mitigating Systems Performance Index (MSPI) - Heat Removal System  
      operator narrative logs, corrective action reports, event reports, MSPI derivation reports,
a.  
      and NRC integrated IRs for October 2008 through June 2009 to validate the accuracy of
Inspection Scope  
      the submittals. The inspectors reviewed the MSPI component risk coefficient to
The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for  
      determine if it had changed by more than 25 percent in value since the previous
Unit 1 and Unit 2 for the third quarter 2008 through the second quarter of 2009.
      inspection, and if so, that the change was in accordance with applicable NEI guidance.
To determine the accuracy of this PI data, definitions and guidance contained in the  
      The inspectors also reviewed the licensee's CAP database to determine if any problems
Nuclear Energy Initiative (NEI) Document 99-02, "Regulatory Assessment Performance  
      had been identified with the PI data collected or transmitted for this indicator.
Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's  
      Documents reviewed are listed in the Attachment to this report.
operator narrative logs, corrective action reports, event reports, MSPI derivation reports,  
      This inspection constituted two MSPI heat removal system samples as defined in
and NRC integrated IRs for October 2008 through June 2009 to validate the accuracy of  
      IP 71151-05.
the submittals. The inspectors reviewed the MSPI component risk coefficient to  
  b. Findings
determine if it had changed by more than 25 percent in value since the previous  
      No findings of significance were identified.
inspection, and if so, that the change was in accordance with applicable NEI guidance.
.2   MSPI - RHR System
The inspectors also reviewed the licensee's CAP database to determine if any problems  
  a. Inspection Scope
had been identified with the PI data collected or transmitted for this indicator.
      The inspectors sampled licensee submittals for the MSPI Index - RHR System PI Unit 1
Documents reviewed are listed in the Attachment to this report.  
      and Unit 2 for the third quarter 2008 through the second quarter of 2009. To determine
This inspection constituted two MSPI heat removal system samples as defined in  
      the accuracy of the PI data, definitions and guidance contained in NEI 99-02, Revision 5,
IP 71151-05.  
      were used. The inspectors reviewed the licensee's operator narrative logs, issue
b.  
      reports, MSPI derivation reports, event reports, and NRC Integrated IRs for October
Findings  
      2008 through June 2009, to validate the accuracy of the submittals. The inspectors
No findings of significance were identified.  
      reviewed the MSPI component risk coefficient to determine if it had changed by more
.2  
      than 25 percent in value since the previous inspection, and if so, that the change was in
MSPI - RHR System  
      accordance with applicable NEI guidance. The inspectors also reviewed the licensee's
a.  
                                                38                                      Enclosure
Inspection Scope  
The inspectors sampled licensee submittals for the MSPI Index - RHR System PI Unit 1  
and Unit 2 for the third quarter 2008 through the second quarter of 2009. To determine  
the accuracy of the PI data, definitions and guidance contained in NEI 99-02, Revision 5,  
were used. The inspectors reviewed the licensee's operator narrative logs, issue  
reports, MSPI derivation reports, event reports, and NRC Integrated IRs for October  
2008 through June 2009, to validate the accuracy of the submittals. The inspectors  
reviewed the MSPI component risk coefficient to determine if it had changed by more  
than 25 percent in value since the previous inspection, and if so, that the change was in  
accordance with applicable NEI guidance. The inspectors also reviewed the licensee's  


    issue report database to determine if any problems had been identified with the PI data
    collected or transmitted for this indicator and none were identified. Documents reviewed
Enclosure
    are listed in the Attachment to this report.
39
    This inspection constituted two MSPI RHR system sample as defined in IP 71151-05.
issue report database to determine if any problems had been identified with the PI data  
  b. Findings
collected or transmitted for this indicator and none were identified. Documents reviewed  
    No findings of significance were identified.
are listed in the Attachment to this report.  
.3   Drill/Exercise Performance
This inspection constituted two MSPI RHR system sample as defined in IP 71151-05.  
  a. Inspection Scope
b.  
    The inspectors sampled licensee submittals for the Drill/Exercise PI for the fourth quarter
Findings  
    2008 through third quarter 2009. To determine the accuracy of the PI data, definitions and
No findings of significance were identified.  
    guidance contained in NEI 99-02, Revision 5, were used. The inspectors reviewed the
.3  
    licensee's records associated with the PI to verify that the licensee accurately reported the
Drill/Exercise Performance  
    PI in accordance with relevant procedures and the NEI guidance. Specifically, the
a.  
    inspectors reviewed licensee records and processes including procedural guidance on
Inspection Scope  
    assessing opportunities for the PI, and assessments of PI opportunities during
The inspectors sampled licensee submittals for the Drill/Exercise PI for the fourth quarter  
    pre-designated control room simulator training sessions, performance during the 2008
2008 through third quarter 2009. To determine the accuracy of the PI data, definitions and  
    biennial exercise, and performance during other drills. Documents reviewed are listed in
guidance contained in NEI 99-02, Revision 5, were used. The inspectors reviewed the  
    the Attachment to this report.
licensee's records associated with the PI to verify that the licensee accurately reported the  
    This inspection constitutes one drill/exercise performance sample as defined in
PI in accordance with relevant procedures and the NEI guidance. Specifically, the  
    IP 71151-05.
inspectors reviewed licensee records and processes including procedural guidance on  
  b. Findings
assessing opportunities for the PI, and assessments of PI opportunities during  
    No findings of significance were identified.
pre-designated control room simulator training sessions, performance during the 2008  
.4   ERO Drill Participation
biennial exercise, and performance during other drills. Documents reviewed are listed in  
  a. Inspection Scope
the Attachment to this report.  
    The inspectors sampled licensee submittals for the ERO Drill Participation PI for the
This inspection constitutes one drill/exercise performance sample as defined in  
    fourth quarter 2008 through third quarter 2009. To determine the accuracy of the PI data,
IP 71151-05.  
    definitions and guidance contained in NEI 99-02, Revision 5, were used. The inspectors
b.  
    reviewed the licensee's records associated with the PI to verify that the licensee
Findings  
    accurately reported the indicator in accordance with relevant procedures and the
No findings of significance were identified.  
    NEI guidance. Specifically, the inspectors reviewed licensee records and processes
.4  
    including procedural guidance on assessing opportunities for the PI; performance during
ERO Drill Participation  
    the 2008 biennial exercise and other drills; and revisions of the roster of personnel
a.  
    assigned to key emergency response organization positions. Documents reviewed are
Inspection Scope  
    listed in the Attachment to this report.
The inspectors sampled licensee submittals for the ERO Drill Participation PI for the  
    This inspection constitutes one ERO drill participation sample as defined in IP 71151-05.
fourth quarter 2008 through third quarter 2009. To determine the accuracy of the PI data,  
                                              39                                      Enclosure
definitions and guidance contained in NEI 99-02, Revision 5, were used. The inspectors  
reviewed the licensee's records associated with the PI to verify that the licensee  
accurately reported the indicator in accordance with relevant procedures and the  
NEI guidance. Specifically, the inspectors reviewed licensee records and processes  
including procedural guidance on assessing opportunities for the PI; performance during  
the 2008 biennial exercise and other drills; and revisions of the roster of personnel  
assigned to key emergency response organization positions. Documents reviewed are  
listed in the Attachment to this report.  
This inspection constitutes one ERO drill participation sample as defined in IP 71151-05.  


  b. Findings
    No findings of significance were identified.
Enclosure
.5   Alert and Notification System
40
  a. Inspection Scope
b.  
    The inspectors sampled licensee submittals for the ANS PI for the fourth quarter 2008
Findings  
    through third quarter 2009. To determine the accuracy of the PI data, definitions and
No findings of significance were identified.  
    guidance contained in NEI 99-02, Revision 5, were used. The inspectors reviewed the
.5  
    licensee's records associated with the PI to verify that the licensee accurately reported the
Alert and Notification System  
    indicator in accordance with relevant procedures and the NEI guidance. Specifically, the
a.  
    inspectors reviewed licensee records and processes including procedural guidance on
Inspection Scope  
    assessing opportunities for the PI and results of periodic ANS operability tests.
The inspectors sampled licensee submittals for the ANS PI for the fourth quarter 2008  
    Documents reviewed are listed in the Attachment to this report.
through third quarter 2009. To determine the accuracy of the PI data, definitions and  
    This inspection constitutes one ANS sample as defined in IP 71151-05.
guidance contained in NEI 99-02, Revision 5, were used. The inspectors reviewed the  
  b. Findings
licensee's records associated with the PI to verify that the licensee accurately reported the  
    No findings of significance were identified.
indicator in accordance with relevant procedures and the NEI guidance. Specifically, the  
.6   Occupational Exposure Control Effectiveness
inspectors reviewed licensee records and processes including procedural guidance on  
  a. Inspection Scope
assessing opportunities for the PI and results of periodic ANS operability tests.
    The inspectors sampled licensee submittals for the Occupational Radiological
Documents reviewed are listed in the Attachment to this report.  
    Occurrences PI for the third quarter 2008 through the third quarter 2009. To determine
This inspection constitutes one ANS sample as defined in IP 71151-05.  
    the accuracy of the PI data, definitions and guidance contained in NEI 99-02,
b.  
    "Regulatory Assessment Performance Indicator Guideline," Revision 6 (issued
Findings  
    October 2009), were used. The inspectors reviewed the licensee's assessment of the
No findings of significance were identified.  
    PI for occupational radiation safety to determine if indicator related data was adequately
.6  
    assessed and reported. To assess the adequacy of the licensee's PI data collection and
Occupational Exposure Control Effectiveness  
    analyses, the inspectors discussed with radiation protection staff the scope and breadth
a.  
    of its data review and the results of those reviews. The inspectors independently
Inspection Scope  
    reviewed electronic dosimetry dose rate and accumulated dose alarm and dose reports
The inspectors sampled licensee submittals for the Occupational Radiological  
    and the dose assignments for any intakes that occurred during the time period reviewed
Occurrences PI for the third quarter 2008 through the third quarter 2009. To determine  
    to determine if there were potentially unrecognized occurrences. The inspectors also
the accuracy of the PI data, definitions and guidance contained in NEI 99-02,  
    conducted walkdowns of locked high and very high radiation area entrances to
"Regulatory Assessment Performance Indicator Guideline," Revision 6 (issued  
    determine the adequacy of the controls in place for these areas. Documents reviewed
October 2009), were used. The inspectors reviewed the licensee's assessment of the  
    are listed in the Attachment to this report.
PI for occupational radiation safety to determine if indicator related data was adequately  
    This inspection constituted one occupational radiological occurrences sample as defined
assessed and reported. To assess the adequacy of the licensee's PI data collection and  
    in IP 71151-05.
analyses, the inspectors discussed with radiation protection staff the scope and breadth  
  b. Findings
of its data review and the results of those reviews. The inspectors independently  
    No findings of significance were identified.
reviewed electronic dosimetry dose rate and accumulated dose alarm and dose reports  
                                              40                                      Enclosure
and the dose assignments for any intakes that occurred during the time period reviewed  
to determine if there were potentially unrecognized occurrences. The inspectors also  
conducted walkdowns of locked high and very high radiation area entrances to  
determine the adequacy of the controls in place for these areas. Documents reviewed  
are listed in the Attachment to this report.  
This inspection constituted one occupational radiological occurrences sample as defined  
in IP 71151-05.  
b.  
Findings  
No findings of significance were identified.  


  .7   Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent
   
      Occurrences
Enclosure
  a. Inspection Scope
41
      The inspectors sampled licensee submittals for the Radiological Effluent TS/Offsite
.7  
      Dose Calculation Manual Radiological Effluent Occurrences PI for the third quarter 2008
Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent  
      through the third quarter 2009. The inspectors used PI definitions and guidance
Occurrences  
      contained in NEI 99-02, Revision 6, to determine the accuracy of the PI data.
a.  
      The inspectors reviewed the licensee's issue report database and selected individual
Inspection Scope  
      reports generated since this indicator was last reviewed to identify any potential
The inspectors sampled licensee submittals for the Radiological Effluent TS/Offsite  
      occurrences such as unmonitored, uncontrolled, or improperly calculated effluent
Dose Calculation Manual Radiological Effluent Occurrences PI for the third quarter 2008  
      releases that may have impacted offsite dose. The inspectors reviewed gaseous
through the third quarter 2009. The inspectors used PI definitions and guidance  
      effluent summary data and the results of associated offsite dose calculations for selected
contained in NEI 99-02, Revision 6, to determine the accuracy of the PI data.
      dates between the third quarter 2008 and the third quarter 2009 to determine if indicator
The inspectors reviewed the licensee's issue report database and selected individual  
      results were accurately reported. The inspectors also reviewed the licensee's methods
reports generated since this indicator was last reviewed to identify any potential  
      for quantifying gaseous and liquid effluents and determining effluent dose. Documents
occurrences such as unmonitored, uncontrolled, or improperly calculated effluent  
      reviewed are listed in the Attachment to this report.
releases that may have impacted offsite dose. The inspectors reviewed gaseous  
      This inspection constituted one radiological effluent technical specification/offsite dose
effluent summary data and the results of associated offsite dose calculations for selected  
      calculation manual radiological effluent occurrences sample as defined in IP 71151-05.
dates between the third quarter 2008 and the third quarter 2009 to determine if indicator  
  b. Findings
results were accurately reported. The inspectors also reviewed the licensee's methods  
      No findings of significance were identified.
for quantifying gaseous and liquid effluents and determining effluent dose. Documents  
4OA2 Identification and Resolution of Problems (71152)
reviewed are listed in the Attachment to this report.  
.1   Routine Review of Items Entered into the CAP
This inspection constituted one radiological effluent technical specification/offsite dose  
  a. Inspection Scope
calculation manual radiological effluent occurrences sample as defined in IP 71151-05.  
      As part of the various baseline IPs discussed in previous sections of this report, the
b.  
      inspectors routinely reviewed issues during baseline inspection activities and plant
Findings  
      status reviews to verify that they were being entered into the licensee's CAP at an
No findings of significance were identified.  
      appropriate threshold, that adequate attention was being given to timely corrective
4OA2 Identification and Resolution of Problems (71152)  
      actions, and that adverse trends were identified and addressed. Attributes reviewed
.1  
      included: the complete and accurate identification of the problem; that timeliness was
Routine Review of Items Entered into the CAP  
      commensurate with the safety significance; that evaluation and disposition of
a.  
      performance issues, generic implications, common causes, contributing factors, root
Inspection Scope  
      causes, extent-of-condition reviews, and previous occurrences reviews were proper and
As part of the various baseline IPs discussed in previous sections of this report, the  
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
inspectors routinely reviewed issues during baseline inspection activities and plant  
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
status reviews to verify that they were being entered into the licensee's CAP at an  
      Minor issues entered into the licensee's CAP as a result of the inspectors' observations
appropriate threshold, that adequate attention was being given to timely corrective  
      are included in the attached List of Documents Reviewed.
actions, and that adverse trends were identified and addressed. Attributes reviewed  
      These routine reviews for the identification and resolution of problems did not constitute
included: the complete and accurate identification of the problem; that timeliness was  
      any additional inspection samples. Instead, by procedure, they were considered an
commensurate with the safety significance; that evaluation and disposition of  
      integral part of the inspections performed during the quarter and documented in
performance issues, generic implications, common causes, contributing factors, root  
      Section 1 of this report.
causes, extent-of-condition reviews, and previous occurrences reviews were proper and  
                                              41                                        Enclosure
adequate; and that the classification, prioritization, focus, and timeliness of corrective  
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
Minor issues entered into the licensee's CAP as a result of the inspectors' observations  
are included in the attached List of Documents Reviewed.  
These routine reviews for the identification and resolution of problems did not constitute  
any additional inspection samples. Instead, by procedure, they were considered an  
integral part of the inspections performed during the quarter and documented in  
Section 1 of this report.  


  b. Findings
    No findings of significance were identified.
Enclosure
.2   Daily CAP Reviews
42
  a. Inspection Scope
b.  
    To assist with the identification of repetitive equipment failures and specific human
Findings  
    performance issues for follow-up, the inspectors performed a daily screening of items
No findings of significance were identified.  
    entered into the licensee's CAP. This review was accomplished through inspection of
.2  
    the station's daily condition report packages.
Daily CAP Reviews  
    These reviews were performed by procedure as part of the inspectors' daily plant status
a.  
    monitoring activities and, as such, did not constitute any separate inspection samples.
Inspection Scope  
  b. Findings
To assist with the identification of repetitive equipment failures and specific human  
    No findings of significance were identified.
performance issues for follow-up, the inspectors performed a daily screening of items  
.3   Semi-Annual Trend Review
entered into the licensee's CAP. This review was accomplished through inspection of  
  a. Inspection Scope
the station's daily condition report packages.  
    The inspectors performed a review of the licensee's CAP and associated documents to
These reviews were performed by procedure as part of the inspectors' daily plant status  
    identify trends that could indicate the existence of a more significant safety issue. The
monitoring activities and, as such, did not constitute any separate inspection samples.  
    inspectors' review was focused on repetitive equipment issues, but also considered the
b.  
    results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
Findings  
    licensee trending efforts, and licensee human performance results. The inspectors'
No findings of significance were identified.  
    review nominally considered the six-month period of July through December 2009,
.3  
    although some examples extended beyond those dates where the scope of the trend
Semi-Annual Trend Review  
    warranted.
a.  
    The review also included issues documented outside the normal CAP in major
Inspection Scope  
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
The inspectors performed a review of the licensee's CAP and associated documents to  
    problem/challenges lists, system health reports, quality assurance audit/surveillance
identify trends that could indicate the existence of a more significant safety issue. The  
    reports, self-assessment reports, and Maintenance Rule evaluations. The inspectors
inspectors' review was focused on repetitive equipment issues, but also considered the  
    compared and contrasted their results with the results contained in the licensee's
results of daily inspector CAP item screening discussed in Section 4OA2.2 above,  
    CAP trending reports. Corrective actions associated with a sample of the issues
licensee trending efforts, and licensee human performance results. The inspectors'  
    identified in the licensee's trending reports were reviewed for adequacy.
review nominally considered the six-month period of July through December 2009,  
    This review constituted a single semi-annual trend inspection sample as defined in
although some examples extended beyond those dates where the scope of the trend  
    IP 71152-05.
warranted.  
  b. Findings
The review also included issues documented outside the normal CAP in major  
    No findings of significance were identified.
equipment problem lists, repetitive and/or rework maintenance lists, departmental  
                                                42                                      Enclosure
problem/challenges lists, system health reports, quality assurance audit/surveillance  
reports, self-assessment reports, and Maintenance Rule evaluations. The inspectors  
compared and contrasted their results with the results contained in the licensee's  
CAP trending reports. Corrective actions associated with a sample of the issues  
identified in the licensee's trending reports were reviewed for adequacy.  
This review constituted a single semi-annual trend inspection sample as defined in  
IP 71152-05.  
b.  
Findings  
No findings of significance were identified.  


4OA5 Other Activities
.1   (Closed) URI 05000266/2009004-01; 05000301/2009004-01, Failure to Control
Enclosure
      Radioactive Material Within the Radiologically Controlled Area Resulting in Unnecessary
43
      Dose to Worker
4OA5 Other Activities  
  a. Inspection Scope
.1  
      The inspectors reviewed additional information, including the licensee's dose
(Closed) URI 05000266/2009004-01; 05000301/2009004-01, Failure to Control  
      assessment, for an incident on May 21, 2009, that involved a contract worker who
Radioactive Material Within the Radiologically Controlled Area Resulting in Unnecessary  
      received unnecessary radiation exposure while performing inspections of the licensee's
Dose to Worker  
      electrical transformers. The inspection was completed through in-office review of
a.  
      documents generated by the licensee. The review included discussions with various
Inspection Scope  
      members of the licensee's staff, both in person and by teleconference. A dose
The inspectors reviewed additional information, including the licensee's dose  
      assessment completed by the licensee's consultant was reviewed and independently
assessment, for an incident on May 21, 2009, that involved a contract worker who  
      validated by NRC staff. Documents reviewed are listed in the Attachment to this report.
received unnecessary radiation exposure while performing inspections of the licensee's  
      This URI is closed.
electrical transformers. The inspection was completed through in-office review of  
  b. Findings
documents generated by the licensee. The review included discussions with various  
      Introduction: A self-revealed finding of very low safety-significance (Green) and an
members of the licensee's staff, both in person and by teleconference. A dose  
      associated NCV of 10 CFR 20.1101(b) was identified for the failure to adequately control
assessment completed by the licensee's consultant was reviewed and independently  
      radioactive material and prevent its inadvertent migration outside the RCA, as required
validated by NRC staff. Documents reviewed are listed in the Attachment to this report.
      by licensee procedure.
This URI is closed.  
      Description: On May 21, 2009, a contract worker alarmed the security gatehouse portal
b.  
      radiation monitors while attempting to exit the protected area following completion of
Findings  
      transformer inspections. The transformers are located outside the RCA but within the
Introduction: A self-revealed finding of very low safety-significance (Green) and an  
      protected area. Investigation by the licensee disclosed that the worker picked-up debris
associated NCV of 10 CFR 20.1101(b) was identified for the failure to adequately control  
      (pieces of unmarked tape wadded-together to the size of a billiard ball) found lying near
radioactive material and prevent its inadvertent migration outside the RCA, as required  
      one of the transformers, placed the debris in the front trouser pocket, and approximately
by licensee procedure.  
      two hours later, after completing assigned work duties, alarmed the radiation monitors
Description: On May 21, 2009, a contract worker alarmed the security gatehouse portal  
      upon attempted egress from the protected area. The ball of tape was subsequently
radiation monitors while attempting to exit the protected area following completion of  
      identified by the licensee to be radioactively contaminated, primarily with cobalt-60.
transformer inspections. The transformers are located outside the RCA but within the  
      The licensee's radiation measurements of the wadded tape ball using portable survey
protected area. Investigation by the licensee disclosed that the worker picked-up debris  
      instruments identified contact gamma and beta dose rates of about 6 mrem/hour and
(pieces of unmarked tape wadded-together to the size of a billiard ball) found lying near  
      500 mrad/hour, respectively. Low levels of contamination were also identified on the
one of the transformers, placed the debris in the front trouser pocket, and approximately  
      workers clothing, some personal items, and left hand. No contamination or other
two hours later, after completing assigned work duties, alarmed the radiation monitors  
      contaminated debris was identified during follow-up surveys in/near the transformers.
upon attempted egress from the protected area. The ball of tape was subsequently  
      The licensee performed an apparent cause evaluation (ACE) that determined the tape
identified by the licensee to be radioactively contaminated, primarily with cobalt-60.
      was likely used to cover the ends of piping or contaminated hoses because one of the
The licensee's radiation measurements of the wadded tape ball using portable survey  
      pieces of tape had a two-inch diameter circular marking. During RFOs, the yard area
instruments identified contact gamma and beta dose rates of about 6 mrem/hour and  
      outside the facade access into the containment building was the transfer point for
500 mrad/hour, respectively. Low levels of contamination were also identified on the  
      materials/equipment into and out of the containment building. The containment building
workers clothing, some personal items, and left hand. No contamination or other  
      equipment hatch was sometimes opened to the environment to facilitate movement of
contaminated debris was identified during follow-up surveys in/near the transformers.  
      equipment and supplies. The licensee surmised that since outage equipment/material
The licensee performed an apparent cause evaluation (ACE) that determined the tape  
      was transferred from the containment building at night and during windy conditions and
was likely used to cover the ends of piping or contaminated hoses because one of the  
      at times when portions of the outdoor RCA barrier fence was removed, the material
pieces of tape had a two-inch diameter circular marking. During RFOs, the yard area  
      could have escaped the licensee's control without notice and blown into the transformer
outside the facade access into the containment building was the transfer point for  
      area.
materials/equipment into and out of the containment building. The containment building  
                                                43                                      Enclosure
equipment hatch was sometimes opened to the environment to facilitate movement of  
equipment and supplies. The licensee surmised that since outage equipment/material  
was transferred from the containment building at night and during windy conditions and  
at times when portions of the outdoor RCA barrier fence was removed, the material  
could have escaped the licensee's control without notice and blown into the transformer  
area.  


The contract worker frequented the site on an approximate monthly basis or less,
spending a few hours to inspect and perform minor maintenance on the licensee's main
Enclosure
power transformers. The individual had not entered an RCA while onsite that day, the
44
work was not governed by a RWP, and the individual was not provided dosimetry. The
The contract worker frequented the site on an approximate monthly basis or less,  
worker's assigned duties did not involve exposure to radiation and the individual should
spending a few hours to inspect and perform minor maintenance on the licensee's main  
not have come into contact with any radioactive material. The individual completed the
power transformers. The individual had not entered an RCA while onsite that day, the  
licensee's Plant Access Training required for unescorted access into the protected area
work was not governed by a RWP, and the individual was not provided dosimetry. The  
but not Radiation Worker Training required for access into RCAs. The licensee had
worker's assigned duties did not involve exposure to radiation and the individual should  
classified the worker as a member of the public, as provided in its Plant Access Training,
not have come into contact with any radioactive material. The individual completed the  
because the individual had no need to enter RCAs and the worker's dose was expected
licensee's Plant Access Training required for unescorted access into the protected area  
to be well within the public dose limits of 10 CFR 20.1301. Consequently, the NRC
but not Radiation Worker Training required for access into RCAs. The licensee had  
concluded that the dose received by the contractor from exposure to the contaminated
classified the worker as a member of the public, as provided in its Plant Access Training,
tape was deemed to be "public dose" as defined in 10 CFR 20.1003.
because the individual had no need to enter RCAs and the worker's dose was expected  
A dose evaluation completed by the licensee's consultant determined that the EDE to
to be well within the public dose limits of 10 CFR 20.1301. Consequently, the NRC  
the worker's thigh from exposure to the contaminated ball of tape was approximately
concluded that the dose received by the contractor from exposure to the contaminated  
one mrem. The evaluation was independently reviewed by NRC staff and found to be
tape was deemed to be "public dose" as defined in 10 CFR 20.1003.  
technically adequate and consistent with guidance provided in NRC Regulatory Issue
A dose evaluation completed by the licensee's consultant determined that the EDE to  
Summary 2003-04, "Use of Effective Dose Equivalent in Place of the Deep Dose
the worker's thigh from exposure to the contaminated ball of tape was approximately  
Equivalent in Dose Assessments." The licensee's corrective action called for expanded
one mrem. The evaluation was independently reviewed by NRC staff and found to be  
radiation protection staff oversight during movement of material in/out of the containment
technically adequate and consistent with guidance provided in NRC Regulatory Issue  
building during outages and for any movement of radioactively contaminated materials in
Summary 2003-04, "Use of Effective Dose Equivalent in Place of the Deep Dose  
outdoor areas. Also, a radiation protection procedure was revised to require a
Equivalent in Dose Assessments." The licensee's corrective action called for expanded  
post-outage walkdown of outdoor RCA boundaries to ensure no material escaped.
radiation protection staff oversight during movement of material in/out of the containment  
Additionally, the licensee planned to construct an enclosure so that storage/transfer of
building during outages and for any movement of radioactively contaminated materials in  
contaminated materials could be performed indoors.
outdoor areas. Also, a radiation protection procedure was revised to require a  
Analysis: The inspectors determined that the failure to adequately control radioactive
post-outage walkdown of outdoor RCA boundaries to ensure no material escaped.
material and prevent its migration outside the RCA was a performance deficiency.
Additionally, the licensee planned to construct an enclosure so that storage/transfer of  
The inspectors concluded that the cause of the performance deficiency was reasonably
contaminated materials could be performed indoors.  
within the licensee's ability to foresee and correct and should have been prevented.
Analysis: The inspectors determined that the failure to adequately control radioactive  
The finding was not subject to traditional enforcement since the incident did not have a
material and prevent its migration outside the RCA was a performance deficiency.
significant or potentially significant safety consequence, did not impact the NRC's ability
The inspectors concluded that the cause of the performance deficiency was reasonably  
to perform its regulatory function, and was not willful.
within the licensee's ability to foresee and correct and should have been prevented.  
In accordance with IMC 0612, the inspectors determined that the finding was more than
The finding was not subject to traditional enforcement since the incident did not have a  
minor because it impacted the program and process attribute of the Public Radiation
significant or potentially significant safety consequence, did not impact the NRC's ability  
Safety Cornerstone and adversely affected the associated cornerstone objective of
to perform its regulatory function, and was not willful.  
ensuring adequate protection of public health and safety from exposure to radiation.
In accordance with IMC 0612, the inspectors determined that the finding was more than  
Specifically, contaminated material with measured dose rates distinguishable from
minor because it impacted the program and process attribute of the Public Radiation  
background escaped the licensee's control outside the RCA and resulted in unnecessary
Safety Cornerstone and adversely affected the associated cornerstone objective of  
radiation exposure to a member of the public that was approximately one percent of the
ensuring adequate protection of public health and safety from exposure to radiation.
public dose limit. The finding was assessed using the Public Radiation Safety-
Specifically, contaminated material with measured dose rates distinguishable from  
Significance Determination Process and determined to be of very low safety significance
background escaped the licensee's control outside the RCA and resulted in unnecessary  
because: (1) it involved a radioactive material control problem that was contrary to
radiation exposure to a member of the public that was approximately one percent of the  
NRC requirements and the licensee's procedure; and (2) the dose impact to a member
public dose limit. The finding was assessed using the Public Radiation Safety-
of the public (the contract worker) was less than 5 mrem total EDE.
Significance Determination Process and determined to be of very low safety significance  
The licensee conducted a "why staircase" analysis as part of its ACE that focused on
because: (1) it involved a radioactive material control problem that was contrary to  
why contaminated equipment was transferred/stored in outdoor areas (a contributor to
NRC requirements and the licensee's procedure; and (2) the dose impact to a member  
                                            44                                  Enclosure
of the public (the contract worker) was less than 5 mrem total EDE.  
The licensee conducted a "why staircase" analysis as part of its ACE that focused on  
why contaminated equipment was transferred/stored in outdoor areas (a contributor to  


    the problem) instead of why material control was compromised in this instance
    (the fundamental cause). Given that the licensee elected to transfer equipment outdoors
Enclosure
    during potentially unfavorable environmental conditions without adequate controls in
45
    place, the cause of the radioactive material control problem was determined to involve a
the problem) instead of why material control was compromised in this instance  
    cross-cutting component in the human performance area for inadequate work control.
(the fundamental cause). Given that the licensee elected to transfer equipment outdoors  
    Specifically, the licensee did not plan/coordinate work activities consistent with safety in
during potentially unfavorable environmental conditions without adequate controls in  
    that job site conditions, including environmental conditions (high winds, night time work,
place, the cause of the radioactive material control problem was determined to involve a  
    etc.), impacted human performance and consequently radiological safety during
cross-cutting component in the human performance area for inadequate work control.
    movement of contaminated material and equipment (H.3.(a)).
Specifically, the licensee did not plan/coordinate work activities consistent with safety in  
    Enforcement: Title 10 CFR 20.1101(b) requires that each licensee use to the extent
that job site conditions, including environmental conditions (high winds, night time work,  
    practical procedures based on sound radiation protection principles to achieve
etc.), impacted human performance and consequently radiological safety during  
    occupational and public doses as low as is reasonably achievable. Licensee procedure
movement of contaminated material and equipment (H.3.(a)).  
    NP 4.2.25, Revision 14, "Release of Material, Equipment and Personal Items From
Enforcement: Title 10 CFR 20.1101(b) requires that each licensee use to the extent  
    Radiologically Controlled Areas," implements 10 CFR 20.1101(b) and was established to
practical procedures based on sound radiation protection principles to achieve  
    ensure that licensed material is controlled and that dose to the public is minimized.
occupational and public doses as low as is reasonably achievable. Licensee procedure  
    Sections 2.1, 2.4, and 4.1 of the procedure require that radioactive material remain in
NP 4.2.25, Revision 14, "Release of Material, Equipment and Personal Items From  
    RCAs, and that contaminated items be monitored by qualified radiation protection
Radiologically Controlled Areas," implements 10 CFR 20.1101(b) and was established to  
    personnel to determine they are free from detectable radioactive contamination prior to
ensure that licensed material is controlled and that dose to the public is minimized.
    release. Contrary to these requirements, on May 21, 2009, radioactively contaminated
Sections 2.1, 2.4, and 4.1 of the procedure require that radioactive material remain in  
    debris escaped the licensee's control, migrated outside the RCA, and was picked-up by
RCAs, and that contaminated items be monitored by qualified radiation protection  
    an individual resulting in unnecessary radiation exposure. Since the failure to control
personnel to determine they are free from detectable radioactive contamination prior to  
    radioactive material was of very low safety significance, corrective actions were
release. Contrary to these requirements, on May 21, 2009, radioactively contaminated  
    proposed as described above, and the issue was entered into the licensee's CAP as
debris escaped the licensee's control, migrated outside the RCA, and was picked-up by  
    AR 01150045, the violation is being treated as an NCV consistent with Section VI.A of
an individual resulting in unnecessary radiation exposure. Since the failure to control  
    the NRC Enforcement Policy (NCV 05000266/2009005-06; 05000301/2009005-06).
radioactive material was of very low safety significance, corrective actions were  
.2   (Closed) NRC TI 2515/175, "Emergency Response Organization, Drill/Exercise
proposed as described above, and the issue was entered into the licensee's CAP as  
    Performance Indicator, Program Review"
AR 01150045, the violation is being treated as an NCV consistent with Section VI.A of  
    The inspectors performed TI 2515/175, ensured the completeness of the TI's
the NRC Enforcement Policy (NCV 05000266/2009005-06; 05000301/2009005-06).  
    Attachment 1, and then forwarded the data to NRC Headquarters.
.2  
.3   (Open) NRC TI 2515/177, "Managing Gas Accumulation in Emergency Core Cooling,
(Closed) NRC TI 2515/175, "Emergency Response Organization, Drill/Exercise  
    Decay Heat Removal and Containment Spray Systems (NRC Generic Letter 2008-01)"
Performance Indicator, Program Review"  
  a. Inspection Scope and Documentation
The inspectors performed TI 2515/175, ensured the completeness of the TI's  
    On October 27, 2009, the inspectors conducted a walkdown of normally inaccessible
Attachment 1, and then forwarded the data to NRC Headquarters.  
    portion of piping of the RHR system in sufficient detail to reasonably assure the
.3  
    acceptability of the licensee's walkdowns (TI 2515/177, Section 04.02.d). The inspectors
(Open) NRC TI 2515/177, "Managing Gas Accumulation in Emergency Core Cooling,  
    also verified that the information obtained during the licensee's walkdown was consistent
Decay Heat Removal and Containment Spray Systems (NRC Generic Letter 2008-01)"  
    with the items identified during the inspectors independent walkdown (TI 2515/177,
a.  
    Section 04.02.c.3).
Inspection Scope and Documentation  
    In addition, the inspectors verified that the licensee had isometric drawings that
On October 27, 2009, the inspectors conducted a walkdown of normally inaccessible  
    described the RHR system configurations. Specifically, the inspectors verified the
portion of piping of the RHR system in sufficient detail to reasonably assure the  
    following, related to the isometric drawings:
acceptability of the licensee's walkdowns (TI 2515/177, Section 04.02.d). The inspectors  
    *       high point vents were identified;
also verified that the information obtained during the licensee's walkdown was consistent  
    *       high points that do not have vents were acceptably recognizable;
with the items identified during the inspectors independent walkdown (TI 2515/177,  
                                                45                                      Enclosure
Section 04.02.c.3).  
In addition, the inspectors verified that the licensee had isometric drawings that  
described the RHR system configurations. Specifically, the inspectors verified the  
following, related to the isometric drawings:  
*  
high point vents were identified;  
*  
high points that do not have vents were acceptably recognizable;  


    *       other areas where gas can accumulate and potentially impact subject system
              operability, such as at orifices in horizontal pipes, isolated branch lines, heat
Enclosure
              exchangers, improperly sloped piping, and under closed valves, were acceptably
46
              described in the drawings or in referenced documentation;
*  
    *       horizontal pipe centerline elevation deviations and pipe slopes in nominally
other areas where gas can accumulate and potentially impact subject system  
              horizontal lines that exceed specified criteria were identified;
operability, such as at orifices in horizontal pipes, isolated branch lines, heat  
    *       all pipes and fittings were clearly shown; and
exchangers, improperly sloped piping, and under closed valves, were acceptably  
    *       the drawings were up-to-date with respect to recent hardware changes and that
described in the drawings or in referenced documentation;  
              any discrepancies between as-built configurations and the drawings were
*  
              documented and entered into the CAP for resolution.
horizontal pipe centerline elevation deviations and pipe slopes in nominally  
    The inspectors noted that the isometric drawings were not accurate with respect to small
horizontal lines that exceed specified criteria were identified;  
    bore piping (TI 2515/177, Section 04.02.a). Specifically, the inspectors found two vent
*  
    valves and one small relief valve that were not shown in the isometric drawings.
all pipes and fittings were clearly shown; and  
    Subsequently, the inspectors were informed by the licensee that the drawings were
*  
    developed to record dimensions and configurations necessary to perform pipe stress
the drawings were up-to-date with respect to recent hardware changes and that  
    analyses and that the scope of that effort excluded piping with a diameter less than
any discrepancies between as-built configurations and the drawings were  
    2.5 inches. Although these specific examples did not present an adverse impact to plant
documented and entered into the CAP for resolution.  
    safety at the time of the inspection, the inspectors questioned if the level of detail of the
The inspectors noted that the isometric drawings were not accurate with respect to small  
    isometric drawings was appropriate with regard to the Gas Accumulation Management
bore piping (TI 2515/177, Section 04.02.a). Specifically, the inspectors found two vent  
    Program. The licensee captured the issue in its CAP as AR 01159839.
valves and one small relief valve that were not shown in the isometric drawings.
    In addition, the inspectors verified that Piping and Instrumentation Diagrams (P&IDs)
Subsequently, the inspectors were informed by the licensee that the drawings were  
    accurately described the subject systems, that they were up-to-date with respect to
developed to record dimensions and configurations necessary to perform pipe stress  
    recent hardware changes, and any discrepancies between as-built configurations, the
analyses and that the scope of that effort excluded piping with a diameter less than  
    isometric drawings, and the P&IDs were documented and entered into the CAP for
2.5 inches. Although these specific examples did not present an adverse impact to plant  
    resolution (TI 2515/177, Section 04.02.b).
safety at the time of the inspection, the inspectors questioned if the level of detail of the  
    Documents reviewed are listed in the Attachment to this report.
isometric drawings was appropriate with regard to the Gas Accumulation Management  
    This inspection effort counts towards the completion of TI 2515/177, which will be closed
Program. The licensee captured the issue in its CAP as AR 01159839.  
    in a later IR.
In addition, the inspectors verified that Piping and Instrumentation Diagrams (P&IDs)  
  b. Findings
accurately described the subject systems, that they were up-to-date with respect to  
    No findings of significance were identified.
recent hardware changes, and any discrepancies between as-built configurations, the  
.4   Confirmatory Order EA-06-178 Actions (92702)
isometric drawings, and the P&IDs were documented and entered into the CAP for  
  a. Inspection Scope
resolution (TI 2515/177, Section 04.02.b).  
    In a letter dated January 3, 2007, (ADAMS Accession Number ML063630336),
Documents reviewed are listed in the Attachment to this report.  
    the NRC issued a Confirmatory Order to the licensee as part of a settlement agreement
This inspection effort counts towards the completion of TI 2515/177, which will be closed  
    through the NRC's Alternative Dispute Resolution (ADR) program. The NRC
in a later IR.  
    investigated an alleged violation of 10 CFR 50.7, "Employee Protection," to determine
b.  
    whether a senior reactor operator was the subject of retaliation for raising a nuclear
Findings  
    safety concern in the licensees CAP. This issue was resolved through the
No findings of significance were identified.  
    NRCs ADR program and was being tracked as Apparent Violation (AV)
.4  
    05000266/2006013-05; 05000301/2006013-05 pending continuing NRC review and
Confirmatory Order EA-06-178 Actions (92702)  
    inspection of the licensees completion of the items specified in the Confirmatory Order.
a.  
                                                46                                        Enclosure
Inspection Scope  
In a letter dated January 3, 2007, (ADAMS Accession Number ML063630336),  
the NRC issued a Confirmatory Order to the licensee as part of a settlement agreement  
through the NRC's Alternative Dispute Resolution (ADR) program. The NRC  
investigated an alleged violation of 10 CFR 50.7, "Employee Protection," to determine  
whether a senior reactor operator was the subject of retaliation for raising a nuclear  
safety concern in the licensees CAP. This issue was resolved through the  
NRCs ADR program and was being tracked as Apparent Violation (AV)  
05000266/2006013-05; 05000301/2006013-05 pending continuing NRC review and  
inspection of the licensees completion of the items specified in the Confirmatory Order.


The Order had been issued to the Nuclear Management Company (NMC), the previous
operator of the Point Beach plant.
Enclosure
From December 14 through 18, 2009, the inspectors utilized IP 92702, "Followup On
47
Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action
The Order had been issued to the Nuclear Management Company (NMC), the previous  
Letters, Confirmatory Orders, And Alternative Dispute Resolution Confirmatory Orders,"
operator of the Point Beach plant.  
to assess the licensees completion of the items contained in the Order. The inspectors
From December 14 through 18, 2009, the inspectors utilized IP 92702, "Followup On  
interviewed site personnel, observed training conducted in response to the Confirmatory
Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action  
Order, performed document reviews, and reviewed some of the applicable corrective
Letters, Confirmatory Orders, And Alternative Dispute Resolution Confirmatory Orders,"  
actions the licensee had taken in response to the Confirmatory Order. An Office of
to assess the licensees completion of the items contained in the Order. The inspectors  
Enforcement Specialist assisted the inspectors.
interviewed site personnel, observed training conducted in response to the Confirmatory  
In addition, the inspectors also assessed the results of the licensees independent
Order, performed document reviews, and reviewed some of the applicable corrective  
assessment of the corrective actions taken in response to the licensees 2004, 2006,
actions the licensee had taken in response to the Confirmatory Order. An Office of  
and 2008 culture surveys. This independent assessment was requested by the
Enforcement Specialist assisted the inspectors.  
NRC Region III Office in the March 4, 2009, Annual Assessment Letter.
In addition, the inspectors also assessed the results of the licensees independent  
The modifications to the facility license as a result of the Confirmatory Order included the
assessment of the corrective actions taken in response to the licensees 2004, 2006,  
following items, in part:
and 2008 culture surveys. This independent assessment was requested by the  
1. By no later than nine (9) months after the issuance of this Confirmatory Order, the
NRC Region III Office in the March 4, 2009, Annual Assessment Letter.  
    Nuclear Management Company (NMC) agrees to review, revise, and communicate
The modifications to the facility license as a result of the Confirmatory Order included the  
    to NMC employees and managers its policy relating to the writing of CAP reports,
following items, in part:  
    and provide training to NMC employees and managers to clarify managements
1. By no later than nine (9) months after the issuance of this Confirmatory Order, the  
    expectation regarding the use of the program with the goal to ensure employees are
Nuclear Management Company (NMC) agrees to review, revise, and communicate  
    not discouraged, or otherwise retaliated or perceived to be retaliated against, for
to NMC employees and managers its policy relating to the writing of CAP reports,  
    using the CAP.
and provide training to NMC employees and managers to clarify managements  
2. By no later than June 30, 2007, NMC agrees to communicate its safety culture policy
expectation regarding the use of the program with the goal to ensure employees are  
    (including safety-conscious work environment (SCWE)) to NMC employees,
not discouraged, or otherwise retaliated or perceived to be retaliated against, for  
    providing employees with the opportunity to ask questions in a live forum.
using the CAP.  
3. By no later than nine (9) months after the issuance of this Confirmatory Order,
    NMC agrees to train its employees holding supervisory positions and higher who
2. By no later than June 30, 2007, NMC agrees to communicate its safety culture policy  
    have not had formal training on SCWE principles within the previous two years of the
(including safety-conscious work environment (SCWE)) to NMC employees,  
    Confirmatory Order. NMC agrees to use a qualified training instructor (internal or
providing employees with the opportunity to ask questions in a live forum.  
    external) for such training. NMC shall review and enhance, if necessary, its
    refresher SCWE training consistent with NMCs refresher training program and
3. By no later than nine (9) months after the issuance of this Confirmatory Order,  
    provide such refresher training to its employees. New employees holding
NMC agrees to train its employees holding supervisory positions and higher who  
    supervisory positions and higher shall be trained on SCWE principles within nine (9)
have not had formal training on SCWE principles within the previous two years of the  
    months of their hire dates unless within the previous two years of their hire dates,
Confirmatory Order. NMC agrees to use a qualified training instructor (internal or  
    they've had the same or equivalent SCWE training.
external) for such training. NMC shall review and enhance, if necessary, its  
4. By no later than March 30, 2007, NMC shall develop action plans to address
refresher SCWE training consistent with NMCs refresher training program and  
    significant issues identified as needing management attention in the NMC 2004 and
provide such refresher training to its employees. New employees holding  
    2006 Comprehensive Cultural Assessments at the Point Beach Nuclear Plant
supervisory positions and higher shall be trained on SCWE principles within nine (9)  
    (PBNP); to conduct focus group interviews with Priority 1 & 2 organizations to
months of their hire dates unless within the previous two years of their hire dates,  
    understand the cause of the survey results; and to review and, as appropriate, reflect
they've had the same or equivalent SCWE training.  
    nuclear industry best practices in its conduct of focus groups and action plans to
    address the issues at PBNP. As part of the development of the action plans,
4. By no later than March 30, 2007, NMC shall develop action plans to address  
    NMC shall also assess and address any legacy issues identified in prior safety
significant issues identified as needing management attention in the NMC 2004 and  
                                          47                                      Enclosure
2006 Comprehensive Cultural Assessments at the Point Beach Nuclear Plant  
(PBNP); to conduct focus group interviews with Priority 1 & 2 organizations to  
understand the cause of the survey results; and to review and, as appropriate, reflect  
nuclear industry best practices in its conduct of focus groups and action plans to  
address the issues at PBNP. As part of the development of the action plans,  
NMC shall also assess and address any legacy issues identified in prior safety  


      culture assessments (i.e., CAP report 0510074 and Synergy Safety Culture
      Assessment) that impact the safety culture at PBNP. The executive summary,
Enclosure
      analysis, and contemplated action plans shall also be submitted to the NRC.
48
  5. By no later than December 31, 2008, NMC shall perform another survey at PBNP
culture assessments (i.e., CAP report 0510074 and Synergy Safety Culture  
      comparable to the 2004 and 2006 surveys to assess trends of the safety culture at
Assessment) that impact the safety culture at PBNP. The executive summary,  
      the site and the overall effectiveness of corrective actions taken in response to prior
analysis, and contemplated action plans shall also be submitted to the NRC.  
      year assessments (i.e., CAP report 0510074 and 2006 Synergy survey).
  6. By no later than 3 months after the receipt of the next cultural survey results at
5. By no later than December 31, 2008, NMC shall perform another survey at PBNP  
      PBNP, NMC shall submit the executive summary, analysis of the results, and the
comparable to the 2004 and 2006 surveys to assess trends of the safety culture at  
      contemplated corrective actions to the NRC.
the site and the overall effectiveness of corrective actions taken in response to prior  
  7. NMC shall continue to implement a process which ensures that adverse employment
year assessments (i.e., CAP report 0510074 and 2006 Synergy survey).  
      actions are in compliance with NRC employee protection regulations and principles
      of SCWE.
6. By no later than 3 months after the receipt of the next cultural survey results at  
  8. In the event of the transfer of the operating license of any NMC operated facility to
PBNP, NMC shall submit the executive summary, analysis of the results, and the  
      another entity, the commitments shall survive for the NMC fleet generally and PBNP
contemplated corrective actions to the NRC.  
      specifically.
b. Observations and Findings
7. NMC shall continue to implement a process which ensures that adverse employment  
  The NRC performed the first inspection of the Confirmatory Order items in June 2007
actions are in compliance with NRC employee protection regulations and principles  
  and documented observations in IR 05000266/2007003; 05000301/2007003, Section
of SCWE.  
  4OA2.3. Inspectors reviewed the licensees completion of Order Items 1, 2, and 3 and
  identified several observations, which the licensee subsequently entered into the CAP as
8. In the event of the transfer of the operating license of any NMC operated facility to  
  AR 01096862.
another entity, the commitments shall survive for the NMC fleet generally and PBNP  
  The second NRC inspection was performed in June 2008 and documented in
specifically.  
  IR 05000266/2008003; 05000301/2008003, Section 4OA5.2. Inspectors verified the
  licensees corrective actions taken in response to the previous NRC observations,
b.  
  documented in AR 01096862; reviewed the SCWE refresher and new supervisor training
Observations and Findings  
  program as required by Order Item 3; and reviewed the licensees actions in response to
The NRC performed the first inspection of the Confirmatory Order items in June 2007  
  Order Item 4. No issues were identified with the actions taken for Order Items 1 and 2,
and documented observations in IR 05000266/2007003; 05000301/2007003, Section  
  and those two items were considered complete. Two Green findings
4OA2.3. Inspectors reviewed the licensees completion of Order Items 1, 2, and 3 and  
  (NCV 05000266/2008003-11; 05000301/2008003-11 and FIN 05000266/2008003-12;
identified several observations, which the licensee subsequently entered into the CAP as  
  05000301/2008003-12) were identified by the inspectors for Order Items 3 and 4, those
AR 01096862.  
  items were not considered complete.
The second NRC inspection was performed in June 2008 and documented in  
  In July 2007, the PBNP operating license was transferred from the NMC to Florida
IR 05000266/2008003; 05000301/2008003, Section 4OA5.2. Inspectors verified the  
  Power and Light (FPL) Energy Point Beach, LLC. In April 2009, FPL Energy Point
licensees corrective actions taken in response to the previous NRC observations,  
  Beach, LLC changed its name to NextEra Energy Point Beach, LLC. Therefore, NextEra
documented in AR 01096862; reviewed the SCWE refresher and new supervisor training  
  Energy Point Beach, LLC assumed responsibility for compliance with the Order.
program as required by Order Item 3; and reviewed the licensees actions in response to  
  The status of the remaining open Order items is summarized below. Note that an item
Order Item 4. No issues were identified with the actions taken for Order Items 1 and 2,  
  status of complete refers to the status of the NRC review and inspection. Order Items 3,
and those two items were considered complete. Two Green findings  
  7, and 8 contain ongoing actions that require continued implementation by the licensee.
(NCV 05000266/2008003-11; 05000301/2008003-11 and FIN 05000266/2008003-12;  
  (Complete) Order Item 3: The licensee continued implementation of Order Item 3, which
05000301/2008003-12) were identified by the inspectors for Order Items 3 and 4, those  
  required, in part, that the licensee provide SCWE training to its employees holding
items were not considered complete.  
                                            48                                    Enclosure
In July 2007, the PBNP operating license was transferred from the NMC to Florida  
Power and Light (FPL) Energy Point Beach, LLC. In April 2009, FPL Energy Point  
Beach, LLC changed its name to NextEra Energy Point Beach, LLC. Therefore, NextEra  
Energy Point Beach, LLC assumed responsibility for compliance with the Order.  
The status of the remaining open Order items is summarized below. Note that an item  
status of complete refers to the status of the NRC review and inspection. Order Items 3,  
7, and 8 contain ongoing actions that require continued implementation by the licensee.  
(Complete) Order Item 3: The licensee continued implementation of Order Item 3, which  
required, in part, that the licensee provide SCWE training to its employees holding  


supervisory positions and higher. The inspectors reviewed AR 01129565, initiated for
NCV 05000266/2008003-11; 05000301/2008003-11, issued in 2008 when the
Enclosure
NRC inspection identified four individuals who did not meet the SCWE training
49
requirement. The four individuals who had exceeded the nine month requirement
supervisory positions and higher. The inspectors reviewed AR 01129565, initiated for  
specified in the Order were subsequently trained by the licensee. In the current
NCV 05000266/2008003-11; 05000301/2008003-11, issued in 2008 when the  
inspection, no additional supervisors were identified that missed the required training.
NRC inspection identified four individuals who did not meet the SCWE training  
The inspectors attended SCWE training for supervisors and found the 2009 training
requirement. The four individuals who had exceeded the nine month requirement  
satisfactory. The inspectors reviewed the licensee procedures and the Learning
specified in the Order were subsequently trained by the licensee. In the current  
Management System and determined they were satisfactory to track personnel for the
inspection, no additional supervisors were identified that missed the required training.
required SCWE training, although the licensee recently identified several issues that
The inspectors attended SCWE training for supervisors and found the 2009 training  
required additional corrective actions. The inspectors determined that these issues,
satisfactory. The inspectors reviewed the licensee procedures and the Learning  
while not performance deficiencies, demonstrated that continued emphasis by the
Management System and determined they were satisfactory to track personnel for the  
licensee was warranted to preclude future performance issues. Some additional
required SCWE training, although the licensee recently identified several issues that  
oversight was provided by the plant training advisory board where, at the monthly
required additional corrective actions. The inspectors determined that these issues,  
meetings, individual supervisors who required SCWE training were tracked.
while not performance deficiencies, demonstrated that continued emphasis by the  
(Complete) Order Item 4: The licensee has completed Order Item 4 concerning actions
licensee was warranted to preclude future performance issues. Some additional  
resulting from the NMC 2004 and 2006 Comprehensive Cultural Assessments. On
oversight was provided by the plant training advisory board where, at the monthly  
March 29, 2007, the licensee submitted to the NRC an analysis of the 2006 culture
meetings, individual supervisors who required SCWE training were tracked.  
survey and the contemplated action plans (ML070890434). The inspectors verified that
(Complete) Order Item 4: The licensee has completed Order Item 4 concerning actions  
the licensee conducted the focus group interviews with Priority 1 and 2 organizations to
resulting from the NMC 2004 and 2006 Comprehensive Cultural Assessments. On  
understand the cause of the survey results, and that nuclear industry best practices were
March 29, 2007, the licensee submitted to the NRC an analysis of the 2006 culture  
reflected in the conduct of focus groups and action plans to address the issues at Point
survey and the contemplated action plans (ML070890434). The inspectors verified that  
Beach.
the licensee conducted the focus group interviews with Priority 1 and 2 organizations to  
The inspectors reviewed the actions and status of the four "quick hitter" plans that were
understand the cause of the survey results, and that nuclear industry best practices were  
identified as not complete in the 2008 NRC inspection and the basis for Finding
reflected in the conduct of focus groups and action plans to address the issues at Point  
05000266/2008003-12; 05000301/2008003-12. The licensee addressed this deficiency
Beach.  
in AR 01129659 and the inspectors verified these "quick hitter" plans were complete.
The inspectors reviewed the actions and status of the four "quick hitter" plans that were  
The inspectors sampled several of the long-term actions plans and verified the licensee
identified as not complete in the 2008 NRC inspection and the basis for Finding  
completed those individual actions. However, the inspectors noted that the results of the
05000266/2008003-12; 05000301/2008003-12. The licensee addressed this deficiency  
2008 safety culture survey (Order Item 5) revealed the overall composite site nuclear
in AR 01129659 and the inspectors verified these "quick hitter" plans were complete.  
safety culture rating remained low and the ratings from 2004 to 2008 showed minimal
The inspectors sampled several of the long-term actions plans and verified the licensee  
improvement. Based on the NRC findings issued in 2008 and the results of the 2008
completed those individual actions. However, the inspectors noted that the results of the  
safety culture survey, the inspectors were concerned there was a lack of management
2008 safety culture survey (Order Item 5) revealed the overall composite site nuclear  
attention and priority to the action plans prior to the 2008 survey and that licensee
safety culture rating remained low and the ratings from 2004 to 2008 showed minimal  
management did not recognize many of the actions taken were either not effective or
improvement. Based on the NRC findings issued in 2008 and the results of the 2008  
could not sustain improvements, especially in the departments which consistently had
safety culture survey, the inspectors were concerned there was a lack of management  
the lowest survey result scores in the 2004, 2006 and 2008 surveys. Licensee actions
attention and priority to the action plans prior to the 2008 survey and that licensee  
taken in response to the 2008 safety culture survey are discussed in the summary for
management did not recognize many of the actions taken were either not effective or  
Order Item 5.
could not sustain improvements, especially in the departments which consistently had  
(Complete) Order Item 5: The licensee has completed Order Item 5, to perform another
the lowest survey result scores in the 2004, 2006 and 2008 surveys. Licensee actions  
survey at PBNP comparable to the 2004 and 2006 surveys. In June 2008, the licensees
taken in response to the 2008 safety culture survey are discussed in the summary for  
contractor conducted a survey at Point Beach and submitted the results of the survey to
Order Item 5.  
the NRC on December 22, 2008, (ML083660387). As previously noted in the Order
(Complete) Order Item 5: The licensee has completed Order Item 5, to perform another  
Item 4 discussion, the survey results did not show a marked improvement from the
survey at PBNP comparable to the 2004 and 2006 surveys. In June 2008, the licensees  
2004/2006 surveys, and Point Beach continued to have an overall low nuclear safety
contractor conducted a survey at Point Beach and submitted the results of the survey to  
culture rating.
the NRC on December 22, 2008, (ML083660387). As previously noted in the Order  
                                          49                                      Enclosure
Item 4 discussion, the survey results did not show a marked improvement from the  
2004/2006 surveys, and Point Beach continued to have an overall low nuclear safety  
culture rating.  


As a result of the 2008 survey, and because the licensee had exceeded three
assessment periods with a substantive cross-cutting issue in problem identification and
Enclosure
resolution, the licensee was requested by the NRC in the March 4, 2009,
50
Annual Assessment Letter to perform an independent assessment of the corrective
As a result of the 2008 survey, and because the licensee had exceeded three  
actions taken in response to the 2004, 2006, and 2008 culture surveys. The
assessment periods with a substantive cross-cutting issue in problem identification and  
independent assessment was performed from June 23 through June 25, 2009.
resolution, the licensee was requested by the NRC in the March 4, 2009,  
The inspectors determined that the assessment team, which consisted of four
Annual Assessment Letter to perform an independent assessment of the corrective  
individuals, was independent from the plant staff, with two members from FPL corporate,
actions taken in response to the 2004, 2006, and 2008 culture surveys. The  
one member from another utility company, and one member from a consultant company.
independent assessment was performed from June 23 through June 25, 2009.
The inspectors noted that the assessment included personnel interviews, meeting
The inspectors determined that the assessment team, which consisted of four  
attendance, and document reviews. The licensees assessment concluded overall that
individuals, was independent from the plant staff, with two members from FPL corporate,  
the corrective actions taken for the 2008 survey results were more effective than those
one member from another utility company, and one member from a consultant company.
taken for the 2004 and 2006 culture surveys, and provided assurance that the progress
The inspectors noted that the assessment included personnel interviews, meeting  
could be sustained. However, the inspectors noted that the report did not include any
attendance, and document reviews. The licensees assessment concluded overall that  
detailed analysis or quantitative data as the basis for the assessments conclusions;
the corrective actions taken for the 2008 survey results were more effective than those  
therefore, the inspectors could not evaluate the assessment teams conclusions. The
taken for the 2004 and 2006 culture surveys, and provided assurance that the progress  
licensees assessment contained six observations and recommendations for
could be sustained. However, the inspectors noted that the report did not include any  
improvements which were:
detailed analysis or quantitative data as the basis for the assessments conclusions;  
    *   an over-reliance on senior managements actions to establish expectations and
therefore, the inspectors could not evaluate the assessment teams conclusions. The  
        demonstrate desired safety culture behaviors; therefore, the team recommended
licensees assessment contained six observations and recommendations for  
        those behaviors be driven down to the department managers and line
improvements which were:  
        organization;
*  
    *   while there is a high level of confidence in the CAP among licensee staff when
an over-reliance on senior managements actions to establish expectations and  
        dealing with safety-related, industrial safety, or plant reliability issues, the same
demonstrate desired safety culture behaviors; therefore, the team recommended  
        confidence level does not exist with lower level issues, especially those which
those behaviors be driven down to the department managers and line  
        are closed to trend; therefore, the team recommended supplemental trending
organization;  
        measures needed to be developed prior to the establishment of a fleet-trending
*  
        program;
while there is a high level of confidence in the CAP among licensee staff when  
    *   while the managers interviewed understood safety culture, those same managers
dealing with safety-related, industrial safety, or plant reliability issues, the same  
        could not clearly articulate a consistent picture of an excellent nuclear safety
confidence level does not exist with lower level issues, especially those which  
        culture; therefore, the team recommended that additional actions be taken to
are closed to trend; therefore, the team recommended supplemental trending  
        ensure the management team could clearly articulate the description of an
measures needed to be developed prior to the establishment of a fleet-trending  
        excellent nuclear safety culture;
program;  
    *   the safety culture effectiveness assessments were currently compliance-focused
*  
        with regard to the completion of corrective actions taken in response to the
while the managers interviewed understood safety culture, those same managers  
        culture surveys; therefore, the team recommended an effectiveness assessment
could not clearly articulate a consistent picture of an excellent nuclear safety  
        be performed to reevaluate the expectations provided in September 2008 and to
culture; therefore, the team recommended that additional actions be taken to  
        promote the day-to-day implementation of the core nuclear safety culture values;
ensure the management team could clearly articulate the description of an  
    *   the organization had difficulty separating day-to-day work place issues from
excellent nuclear safety culture;  
        nuclear safety culture issues; therefore, the team recommended addressing
*  
        day-to-day work place issues in a different forum; and
the safety culture effectiveness assessments were currently compliance-focused  
    *   one of the major focus areas from the 2008 culture survey was achieving a better
with regard to the completion of corrective actions taken in response to the  
        balance between workload and available resources, with the extended power
culture surveys; therefore, the team recommended an effectiveness assessment  
        uprate project adding additional workload to the plant; therefore, the team
be performed to reevaluate the expectations provided in September 2008 and to  
        recommended the extended power uprate project should look for more effective
promote the day-to-day implementation of the core nuclear safety culture values;  
        means of implementation, to avoid unnecessary disruptions of the normal plant
*  
        work schedule.
the organization had difficulty separating day-to-day work place issues from  
                                          50                                          Enclosure
nuclear safety culture issues; therefore, the team recommended addressing  
day-to-day work place issues in a different forum; and  
*  
one of the major focus areas from the 2008 culture survey was achieving a better  
balance between workload and available resources, with the extended power  
uprate project adding additional workload to the plant; therefore, the team  
recommended the extended power uprate project should look for more effective  
means of implementation, to avoid unnecessary disruptions of the normal plant  
work schedule.  


The independent assessment recommendations were entered into the CAP system as
AR 01152228.
Enclosure
The inspectors also reviewed a sample of the corrective actions taken for the
51
weaknesses identified in the 2008 safety culture survey and interviewed personnel in the
The independent assessment recommendations were entered into the CAP system as  
groups having the lowest ratings in the survey. Many of the licensee personnel
AR 01152228.  
interviewed in December 2009 were interviewed during the 2007 and/or 2008 NRC
The inspectors also reviewed a sample of the corrective actions taken for the  
inspections. The inspectors observed that many of the actions were recently completed
weaknesses identified in the 2008 safety culture survey and interviewed personnel in the  
and some groups made significant improvement, while other groups have shown
groups having the lowest ratings in the survey. Many of the licensee personnel  
marginal improvement, if any. However, the inspectors noted that the Point Beach
interviewed in December 2009 were interviewed during the 2007 and/or 2008 NRC  
Nuclear Safety Culture Improvement Team (NSCIT) developed and issued SCWE
inspections. The inspectors observed that many of the actions were recently completed  
performance indicators for all work groups and that those indicators reflected that some
and some groups made significant improvement, while other groups have shown  
groups remained as outliers (needed improvement). Those indicators aligned with the
marginal improvement, if any. However, the inspectors noted that the Point Beach  
NRC observations from day-to-day resident inspections and interviews conducted with
Nuclear Safety Culture Improvement Team (NSCIT) developed and issued SCWE  
licensee personnel during this inspection.
performance indicators for all work groups and that those indicators reflected that some  
In addition, the inspectors reviewed the results of other surveys performed on aspects of
groups remained as outliers (needed improvement). Those indicators aligned with the  
safety culture by FPL in late 2008 and one performed by an independent organization
NRC observations from day-to-day resident inspections and interviews conducted with  
made up of external utility representatives in early 2009. While the inspectors concluded
licensee personnel during this inspection.  
that those surveys were not comparable to the licensees safety culture surveys
In addition, the inspectors reviewed the results of other surveys performed on aspects of  
previously discussed, the inspectors noted that both surveys contained positive results
safety culture by FPL in late 2008 and one performed by an independent organization  
related to the nuclear safety culture and safety conscious work environment at
made up of external utility representatives in early 2009. While the inspectors concluded  
Point Beach, indicative of some improvement since the 2008 safety culture survey.
that those surveys were not comparable to the licensees safety culture surveys  
Therefore, the inspectors concluded that the safety culture environment has shown
previously discussed, the inspectors noted that both surveys contained positive results  
some improvement and further monitoring by the plant NSCIT and continuing actions
related to the nuclear safety culture and safety conscious work environment at  
from the safety culture surveys and independent assessment team recommendations
Point Beach, indicative of some improvement since the 2008 safety culture survey.  
would be needed to continue this trend.
Therefore, the inspectors concluded that the safety culture environment has shown  
(Complete) Order Item 6: The licensee completed Order Item 6 when the licensee
some improvement and further monitoring by the plant NSCIT and continuing actions  
submitted the 2008 Safety Culture Survey executive summary, analysis of the results,
from the safety culture surveys and independent assessment team recommendations  
and the contemplated corrective actions to the NRC on December 22, 2008,
would be needed to continue this trend.  
(ML083660387). The inspectors verified these submittals were complete within the
(Complete) Order Item 6: The licensee completed Order Item 6 when the licensee  
timeframe contained in the Order.
submitted the 2008 Safety Culture Survey executive summary, analysis of the results,  
(Complete) Order Item 7: The licensee continued implementation of Order Item 7 to
and the contemplated corrective actions to the NRC on December 22, 2008,  
implement a process that ensured adverse employment actions were in compliance with
(ML083660387). The inspectors verified these submittals were complete within the  
NRC employee protection regulations and principles of SCWE. The FPL Nuclear
timeframe contained in the Order.  
Division Policy, NP-413, was put in effect on May 15, 2008, and replaced the
(Complete) Order Item 7: The licensee continued implementation of Order Item 7 to  
NMC procedure CP-0087. However, the inspectors observed that the FPL procedure
implement a process that ensured adverse employment actions were in compliance with  
was not as detailed as the original NMC procedure, and a follow-up inspection would be
NRC employee protection regulations and principles of SCWE. The FPL Nuclear  
needed to look at specific adverse action cases. The licensee captured the inspectors
Division Policy, NP-413, was put in effect on May 15, 2008, and replaced the  
observations in condition report AR 01163410.
NMC procedure CP-0087. However, the inspectors observed that the FPL procedure  
In a follow-up inspection, the inspectors reviewed a sample of adverse actions taken at
was not as detailed as the original NMC procedure, and a follow-up inspection would be  
PBNP since policy NP-413 was implemented to ensure the Order requirements were
needed to look at specific adverse action cases. The licensee captured the inspectors  
maintained. The inspectors also reviewed a new FPL Policy, HR-AA-01, Involuntary
observations in condition report AR 01163410.  
Termination or Other Significant Employment Actions Affecting Nuclear Division
In a follow-up inspection, the inspectors reviewed a sample of adverse actions taken at  
Employees, issued as a result of the inspectors previous observations. This new policy
PBNP since policy NP-413 was implemented to ensure the Order requirements were  
contained the employee protection criteria that were missing from the previous policy.
maintained. The inspectors also reviewed a new FPL Policy, HR-AA-01, Involuntary  
During review of a sample of 10 adverse actions, the inspectors identified that in one
Termination or Other Significant Employment Actions Affecting Nuclear Division  
                                        51                                      Enclosure
Employees, issued as a result of the inspectors previous observations. This new policy  
contained the employee protection criteria that were missing from the previous policy.
During review of a sample of 10 adverse actions, the inspectors identified that in one  


    case the licensee had not completed an independent review of the personnel action by
    the Human Resources Department as required by the policy. The licensee entered this
Enclosure
    performance deficiency into the CAP as AR 01165164, performed the independent
52
    review, and determined there were no employee protection issues involved. The
case the licensee had not completed an independent review of the personnel action by  
    inspectors agreed with this determination and concluded the failure to implement the
the Human Resources Department as required by the policy. The licensee entered this  
    FPL Policy was considered a minor violation, in accordance with the NRCs Enforcement
performance deficiency into the CAP as AR 01165164, performed the independent  
    Policy.
review, and determined there were no employee protection issues involved. The  
    (Complete) Order Item 8: For Order Item 8, the inspectors verified that after the transfer
inspectors agreed with this determination and concluded the failure to implement the  
    of the operating license of PBNP from NMC to NextEra Energy (formerly FPL),
FPL Policy was considered a minor violation, in accordance with the NRCs Enforcement  
    PBNP continued to follow the Order commitments.
Policy.  
    No findings of significance were identified during this inspection.
(Complete) Order Item 8: For Order Item 8, the inspectors verified that after the transfer  
    Based on the results of this inspection and the actions documented in IRs
of the operating license of PBNP from NMC to NextEra Energy (formerly FPL),  
    05000266/2007003; 05000301/2007003 and 05000266/2008003; 05000301/2008003,
PBNP continued to follow the Order commitments.  
    the inspectors concluded that the licensee had implemented all the actions required by
No findings of significance were identified during this inspection.  
    the Confirmatory Order (EA-06-178). Therefore, the inspectors considered the
Based on the results of this inspection and the actions documented in IRs  
    associated Apparent Violation 05000266/2006013-05; 05000301/2006013-05,
05000266/2007003; 05000301/2007003 and 05000266/2008003; 05000301/2008003,  
    "Confirmatory Order EA-06-178," closed.
the inspectors concluded that the licensee had implemented all the actions required by  
.5   Plant Modifications in Support of Extended Power Uprate (EPU) (71004)
the Confirmatory Order (EA-06-178). Therefore, the inspectors considered the  
  a. Inspection Scope
associated Apparent Violation 05000266/2006013-05; 05000301/2006013-05,  
    From November 30 through December 18, 2009, the inspectors reviewed the following
"Confirmatory Order EA-06-178," closed.  
    completed plant modifications during a baseline inspection for Evaluations of Changes,
.5  
    Tests, or Experiments and Permanent Plant Modifications. The following two
Plant Modifications in Support of Extended Power Uprate (EPU) (71004)  
    modifications were completed for the Extended Power Uprate project, hence may be
a.  
    also be credited as samples towards completion of IP 71004, Power Uprate. Additional
Inspection Scope  
    details of these samples are included in IR 05000266/2009007; 05000301/2009007.
From November 30 through December 18, 2009, the inspectors reviewed the following  
    *       Mechanical tie-ins to the SW and AFW systems for the new Unit 2 motor-driven
completed plant modifications during a baseline inspection for Evaluations of Changes,  
            AFW pump. Specifically, the inspectors reviewed a sample of the associated
Tests, or Experiments and Permanent Plant Modifications. The following two  
            engineering change documentation, including the 10 CFR 50.59 screening,
modifications were completed for the Extended Power Uprate project, hence may be  
            design calculations, work orders, engineering change requests, and corrective
also be credited as samples towards completion of IP 71004, Power Uprate. Additional  
            action documents, to assure the installed plant change was consistent with the
details of these samples are included in IR 05000266/2009007; 05000301/2009007.  
            design and licensing bases. The inspectors walked down the mechanical tie-ins
*  
            to the SW and feedwater systems to verify the installed piping configurations
Mechanical tie-ins to the SW and AFW systems for the new Unit 2 motor-driven  
            were consistent with the design and installation documentation.
AFW pump. Specifically, the inspectors reviewed a sample of the associated  
    *       Electrical and instrumentation tie-ins installed during the refueling outage for the
engineering change documentation, including the 10 CFR 50.59 screening,  
            new Unit 2 motor-driven AFW pump per EC-13401. The inspectors walked down
design calculations, work orders, engineering change requests, and corrective  
            changes to the Unit 2 control room panels with the SQUG engineer.
action documents, to assure the installed plant change was consistent with the  
  b. Findings
design and licensing bases. The inspectors walked down the mechanical tie-ins  
    No findings of significance were identified.
to the SW and feedwater systems to verify the installed piping configurations  
                                              52                                        Enclosure
were consistent with the design and installation documentation.  
*  
Electrical and instrumentation tie-ins installed during the refueling outage for the  
new Unit 2 motor-driven AFW pump per EC-13401. The inspectors walked down  
changes to the Unit 2 control room panels with the SQUG engineer.  
b.  
Findings  
No findings of significance were identified.  


4OA6 Management Meetings
.1 Exit Meeting Summary
Enclosure
    On January 5, 2010, the inspectors presented the inspection results to Mr. C. Trezise,
53
    and other members of the licensee staff. The licensee acknowledged the issues
4OA6 Management Meetings  
    presented. The inspectors confirmed that none of the potential report input discussed
.1  
    was considered proprietary.
Exit Meeting Summary  
.2 Interim Exit Meetings
On January 5, 2010, the inspectors presented the inspection results to Mr. C. Trezise,  
    Interim exits were conducted for:
and other members of the licensee staff. The licensee acknowledged the issues  
    *       The Occupational Radiation Safety access control to radiologically significant
presented. The inspectors confirmed that none of the potential report input discussed  
              areas and ALARA program inspection results to Mr. L. Meyer and other members
was considered proprietary.  
              of the licensee staff on October 30, 2009. This included closure of URI
.2  
              05000266/2009004-01; 05000301/2009004-01 documented in Section 4OA5.
Interim Exit Meetings  
    *       TI 2515/177 inspection results to Mr. L. Meyer and other members of the
Interim exits were conducted for:  
              licensee staff on October 30, 2009. The licensee acknowledged the issues
*  
              presented.
The Occupational Radiation Safety access control to radiologically significant  
    *       The ISI inspection results to Mr. L. Meyer and other members of the licensee
areas and ALARA program inspection results to Mr. L. Meyer and other members  
              staff on November 6, 2009. The licensee acknowledged the issues presented.
of the licensee staff on October 30, 2009. This included closure of URI  
    *       The Verification of the Public Radiation Safety Performance Indicator inspection
05000266/2009004-01; 05000301/2009004-01 documented in Section 4OA5.  
              results with Mr. J. Pierce on December 4, 2009.
*  
    *       The results of the Emergency Preparedness program inspection with
TI 2515/177 inspection results to Mr. L. Meyer and other members of the  
              Mr. C. Trezise on December 11, 2009.
licensee staff on October 30, 2009. The licensee acknowledged the issues  
    *       The licensed operator requalification training program inspection results with the
presented.  
              Training Operations Supervisor, Mr. R. Amundson, on December 15, 2009.
*  
    *       The annual review of Emergency Action Level and Emergency Plan changes
The ISI inspection results to Mr. L. Meyer and other members of the licensee  
              with the licensee's Emergency Preparedness Manager, Mr. R. Johnson, via
staff on November 6, 2009. The licensee acknowledged the issues presented.  
              telephone on December 15, 2009.
*  
    *       The Confirmatory Order (EA-06-178) inspection results to Mr. L. Meyer and other
The Verification of the Public Radiation Safety Performance Indicator inspection  
              members of the licensee staff on December 18, 2009. The licensee
results with Mr. J. Pierce on December 4, 2009.  
              acknowledged the conclusions and observations presented.
*  
    The inspectors confirmed that none of the potential report input discussed was
The results of the Emergency Preparedness program inspection with  
    considered proprietary. Proprietary material received during the inspection was returned
Mr. C. Trezise on December 11, 2009.  
    to the licensee.
*  
ATTACHMENT: SUPPLEMENTAL INFORMATION
The licensed operator requalification training program inspection results with the  
                                              53                                      Enclosure
Training Operations Supervisor, Mr. R. Amundson, on December 15, 2009.  
*  
The annual review of Emergency Action Level and Emergency Plan changes  
with the licensee's Emergency Preparedness Manager, Mr. R. Johnson, via  
telephone on December 15, 2009.  
*  
The Confirmatory Order (EA-06-178) inspection results to Mr. L. Meyer and other  
members of the licensee staff on December 18, 2009. The licensee  
acknowledged the conclusions and observations presented.  
The inspectors confirmed that none of the potential report input discussed was  
considered proprietary. Proprietary material received during the inspection was returned  
to the licensee.  
ATTACHMENT: SUPPLEMENTAL INFORMATION


                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
1
Licensee
Attachment
S. Aerts, Accounting Manager (NSCIT Leader)
SUPPLEMENTAL INFORMATION  
B. Castiglia, Performance Improvement Manager
KEY POINTS OF CONTACT  
J. Costedio, Nuclear Licensing Manager/Regulatory Affairs Manager
Licensee  
R. Farrell, Radiation Protection Manager
S. Aerts, Accounting Manager (NSCIT Leader)  
R. Freeman, Emergency Preparedness Manager
B. Castiglia, Performance Improvement Manager  
R. Harrsch, Operations Site Director
J. Costedio, Nuclear Licensing Manager/Regulatory Affairs Manager  
L. Hawkeye, Engineering PI Manager
R. Farrell, Radiation Protection Manager  
C. Hill, Work Control Center Manager
R. Freeman, Emergency Preparedness Manager  
P. Holzman, GL 89-13 Program Engineer
R. Harrsch, Operations Site Director  
L. Meyer, Site Vice-President
L. Hawkeye, Engineering PI Manager  
J. Schroeder, SW System Engineer
C. Hill, Work Control Center Manager  
C. Trezise, Engineering Director/Acting Site Vice-President
P. Holzman, GL 89-13 Program Engineer  
T. Vehec, Plant Manager
L. Meyer, Site Vice-President  
G. Vickery, Work Management Manager
J. Schroeder, SW System Engineer  
Nuclear Regulatory Commission
C. Trezise, Engineering Director/Acting Site Vice-President  
M. Kunowski, Chief, Division of Reactor Projects, Branch 5
T. Vehec, Plant Manager  
J. Poole, Point Beach Project Manager, Office of Nuclear Reactor Regulations
G. Vickery, Work Management Manager  
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Nuclear Regulatory Commission  
Opened
M. Kunowski, Chief, Division of Reactor Projects, Branch 5  
05000266/2009005-01;             Failure to Meet GL 89-13 Program for Mussel Control
J. Poole, Point Beach Project Manager, Office of Nuclear Reactor Regulations  
                            FIN
05000301/2009005-01              (Section 1R12.1)
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED  
05000301/2009005-02               Failure to Ensure Adequate Control of Foreign Material in
Opened  
                            NCV
05000266/2009005-01;  
                                  Safety-Related Systems (Section 1R15.1)
05000301/2009005-01
05000301/2009005-03               Failure to Update Safe Load Path Manual to Include
FIN
                            NCV
Failure to Meet GL 89-13 Program for Mussel Control  
                                  Safety-Related Cable Locations (Section 1R18.1)
(Section 1R12.1)  
05000266/2009005-04;             Potential Failure to Adequately Evaluate Seismic II/I
05000301/2009005-02  
05000301/2009005-04        URI  Concerns for Units 1 and 2 'B' Containment Sump Strainers
NCV Failure to Ensure Adequate Control of Foreign Material in  
                                  (Section 1R18.2)
Safety-Related Systems (Section 1R15.1)  
05000301/2009005-05               Momentary Loss of Unit 2 Reactor Vessel Level Indication in
05000301/2009005-03  
                            NCV
NCV Failure to Update Safe Load Path Manual to Include  
                                  the Control Room (Section 1R20.1)
Safety-Related Cable Locations (Section 1R18.1)  
05000266/2009005-06;             Failure to Maintain Proper Control of Radioactive Material
05000266/2009005-04;  
                            NCV
05000301/2009005-04
05000301/2009005-06              Within the Radiologically Controlled Area (Section 4OA5.1)
URI
                                              1                                    Attachment
Potential Failure to Adequately Evaluate Seismic II/I  
Concerns for Units 1 and 2 'B' Containment Sump Strainers
(Section 1R18.2)  
05000301/2009005-05  
NCV Momentary Loss of Unit 2 Reactor Vessel Level Indication in  
the Control Room (Section 1R20.1)  
05000266/2009005-06;  
05000301/2009005-06
NCV Failure to Maintain Proper Control of Radioactive Material  
Within the Radiologically Controlled Area (Section 4OA5.1)  


Closed
05000266/2009005-01;     Failure to Meet GL 89-13 Program Requirement for Mussel
2
                    FIN
Attachment
05000301/2009005-01      Control (Section 1R12.1)
05000301/2009005-02     Failure to Ensure Adequate Control of Foreign Material in
Closed  
                    NCV
05000266/2009005-01;  
                        Safety-Related Systems (Section 1R15.1)
05000301/2009005-01
05000301/2009005-03     Failure to Update Safe Load Path Manual to Include
FIN
                    NCV
Failure to Meet GL 89-13 Program Requirement for Mussel  
                        Safety-Related Cable Locations (Section 1R18.1)
Control (Section 1R12.1)  
05000301/2009005-05     Momentary Loss of Unit 2 Reactor Vessel Level Indication in
05000301/2009005-02  
                    NCV
NCV Failure to Ensure Adequate Control of Foreign Material in  
                        the Control Room (Section 1R20.1)
Safety-Related Systems (Section 1R15.1)  
05000266/2009004-01;     Failure to Control Radioactive Material Within the
05000301/2009005-03  
05000301/2009004-01  URI Radiologically Controlled Area Resulting in Unnecessary
NCV Failure to Update Safe Load Path Manual to Include  
                        Dose to Worker (Section 4OA5.1)
Safety-Related Cable Locations (Section 1R18.1)  
05000266/2009005-06;     Failure to Maintain Proper Control of Radioactive Material
05000301/2009005-05  
                    NCV
NCV Momentary Loss of Unit 2 Reactor Vessel Level Indication in  
05000301/2009005-06      Within the Radiologically Controlled Area (Section 4OA5.1)
the Control Room (Section 1R20.1)  
05000266/2006013-05;     Confirmatory Order EA-06-178 (Section 4OA5.4)
05000266/2009004-01;  
                      AV
05000301/2009004-01
05000301/2006013-05
URI
                                    2                                      Attachment
Failure to Control Radioactive Material Within the  
Radiologically Controlled Area Resulting in Unnecessary  
Dose to Worker (Section 4OA5.1)  
05000266/2009005-06;  
05000301/2009005-06
NCV Failure to Maintain Proper Control of Radioactive Material  
Within the Radiologically Controlled Area (Section 4OA5.1)  
05000266/2006013-05;  
05000301/2006013-05
AV
Confirmatory Order EA-06-178 (Section 4OA5.4)  


                                  LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
3
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
Attachment
selected sections of portions of the documents were evaluated as part of the overall inspection
LIST OF DOCUMENTS REVIEWED  
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
The following is a list of documents reviewed during the inspection. Inclusion on this list does  
any part of it, unless this is stated in the body of the IR.
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that  
1R01 Adverse Weather Protection
selected sections of portions of the documents were evaluated as part of the overall inspection  
- AR 00509533; O&MR 379; Revision 1 Freezing Of Instrumentation Piping
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
- AR 00509586; Reduced Pump Seal Life Because Of Improper Venting
any part of it, unless this is stated in the body of the IR.  
- AR 01075828; PAB HV Steam Exhaust Stack Drain Line Is Frozen
1R01 Adverse Weather Protection  
- AR 01140416; Ice In Sealtite For Many Security Components
- AR 00509533; O&MR 379; Revision 1 Freezing Of Instrumentation Piping  
- AR 01140633; Beach Drains Frozen
- AR 00509586; Reduced Pump Seal Life Because Of Improper Venting  
- AR 01141214; Ice On Floor In Unit 1 Facade
- AR 01075828; PAB HV Steam Exhaust Stack Drain Line Is Frozen  
- AR 01141395; EC 12789 Facade Freeze Upgrade DRB Action items
- AR 01140416; Ice In Sealtite For Many Security Components  
- AR 01141687; Verify Cold Weather Preps Remains In A Working Stat
- AR 01140633; Beach Drains Frozen  
- AR 01142302; U2 Facade Sump Piping Heat Trace Alarms
- AR 01141214; Ice On Floor In Unit 1 Facade  
- AR 01142711; Inadequate 2X04 Cable Drip Tray Causes Ice Buildup In Facade
- AR 01141395; EC 12789 Facade Freeze Upgrade DRB Action items  
- AR 01142806; Changes To OI 106 To Incorporate EC 12789 Facade Freeze Mod
- AR 01141687; Verify Cold Weather Preps Remains In A Working Stat  
- AR 01143674; Faulted MUX Causing MET Tower Data To Be Frozen
- AR 01142302; U2 Facade Sump Piping Heat Trace Alarms  
- AR 01143775; Frozen Drain Line In Unit 2 Facade
- AR 01142711; Inadequate 2X04 Cable Drip Tray Causes Ice Buildup In Facade  
- AR 01146740; Cold Weather Checks UNSAT - Heat Lamp GFI Tripped
- AR 01142806; Changes To OI 106 To Incorporate EC 12789 Facade Freeze Mod  
- AR 01148041; Heat Trace Drawing Needs Updating
- AR 01143674; Faulted MUX Causing MET Tower Data To Be Frozen  
- AR 01148221; Facade Heat Trace Panel reliability Unsatisfactory
- AR 01143775; Frozen Drain Line In Unit 2 Facade  
- AR 01148314; Heat Trace Drawing Needs Updating/More Information
- AR 01146740; Cold Weather Checks UNSAT - Heat Lamp GFI Tripped  
- AR 00149677; Massive Formation Of Ice Has Collected On Cable Tray In Southwest Corner
- AR 01148041; Heat Trace Drawing Needs Updating  
  Of Unit
- AR 01148221; Facade Heat Trace Panel reliability Unsatisfactory  
- AR 01154068; Heat Trace For RS-SA-003 Installed Incorrectly
- AR 01148314; Heat Trace Drawing Needs Updating/More Information  
- AR 01155627; PC 49.5 Cold Weather Checklist, WH4 Heaters Broke
- AR 00149677; Massive Formation Of Ice Has Collected On Cable Tray In Southwest Corner  
- AR 01155718; Heat Trace Not Installed Per Manufacturer Recommendations
Of Unit  
- AR 01155829; Cold Weather Preps
- AR 01154068; Heat Trace For RS-SA-003 Installed Incorrectly  
- AR 01156747; Cold Weather Preps May Not Get Completed As Scheduled
- AR 01155627; PC 49.5 Cold Weather Checklist, WH4 Heaters Broke  
- AR 01156940; Facade Freeze Tent
- AR 01155718; Heat Trace Not Installed Per Manufacturer Recommendations  
- AR 01156958; HV Piping Leak Downstream Of HV-990
- AR 01155829; Cold Weather Preps  
- AR 01157478; CWPH MOD EC 11174 Requires Cold Weather Procedure Update
- AR 01156747; Cold Weather Preps May Not Get Completed As Scheduled  
- AR 01158201; Cold Weather Issue - Primary And Backup Circuit In Alarm
- AR 01156940; Facade Freeze Tent  
- AR 01158202; Cold Weather Issue - Primary And Backup Circuit In Alarm
- AR 01156958; HV Piping Leak Downstream Of HV-990  
- AR 01158203; Cold Weather Issue - Vent To Atmosphere For RWST
- AR 01157478; CWPH MOD EC 11174 Requires Cold Weather Procedure Update  
- AR 01158938; Cold Weather Readiness System Engineering Reviews
- AR 01158201; Cold Weather Issue - Primary And Backup Circuit In Alarm  
- AR 01159535; BDE May Need Cold Weather Shutdown
- AR 01158202; Cold Weather Issue - Primary And Backup Circuit In Alarm  
- AR 01154813; Facade Freeze Protection Work Not Ready
- AR 01158203; Cold Weather Issue - Vent To Atmosphere For RWST  
- AR 01154683; Section Of Facade Heat Tracing Is Missing
- AR 01158938; Cold Weather Readiness System Engineering Reviews  
- AR 01155829; Cold Weather Preps
- AR 01159535; BDE May Need Cold Weather Shutdown  
- ICI 32; Facade Freeze Control Panel Settings; Revision 1
- AR 01154813; Facade Freeze Protection Work Not Ready  
- IE Bulletin 79-24; Frozen Lines; September 27, 1979
- AR 01154683; Section Of Facade Heat Tracing Is Missing  
- ISA-S67.02; Nuclear Safety-Related Instrument Sensing Line Piping And Tubing Standards
- AR 01155829; Cold Weather Preps  
  For Use In Nuclear Power Plants
- ICI 32; Facade Freeze Control Panel Settings; Revision 1  
- OP-AA-102-1002; Seasonal Readiness; Revision 0
- IE Bulletin 79-24; Frozen Lines; September 27, 1979  
- OM 3.39; Degraded Equipment / Adverse Condition Monitoring Procedure; Revision 2
- ISA-S67.02; Nuclear Safety-Related Instrument Sensing Line Piping And Tubing Standards  
                                                  3                                    Attachment
For Use In Nuclear Power Plants  
- OP-AA-102-1002; Seasonal Readiness; Revision 0  
- OM 3.39; Degraded Equipment / Adverse Condition Monitoring Procedure; Revision 2  


- 0-SOP HT-1B01; Unit 1 Non-Vital Train A Heat Trace Panels; Revision 0
- OM 3.9; Watchstation Status Checks And Watchstander Turnover Guides; Revision 15
4
- OI 106; Facade Freeze Protection; Revision 26
Attachment
- OP-AA-102-1002; Seasonal Readiness; Revision 0
- 0-SOP HT-1B01; Unit 1 Non-Vital Train A Heat Trace Panels; Revision 0  
- PC 49; Cold Weather Preparations; Revision 7
- OM 3.9; Watchstation Status Checks And Watchstander Turnover Guides; Revision 15  
- PC 49 Part 5; Cold Weather Checklist: Outside Areas And Miscellaneous; Revision 25
- OI 106; Facade Freeze Protection; Revision 26  
- WO #353856-07; Install 2FF-07-02C Heat Trace Cable On RS-SA-003 And Test
- OP-AA-102-1002; Seasonal Readiness; Revision 0  
- WO #366472; 2VNTB-04802A Damper Not Fully Closing
- PC 49; Cold Weather Preparations; Revision 7  
- Drawing 019193; Electrical Layout Facade Area E-142; Unit 1
- PC 49 Part 5; Cold Weather Checklist: Outside Areas And Miscellaneous; Revision 25  
- Drawing 55805; Wiring Diagram Heat Tracing Panel "AH"; Auxiliary Building; Units 1 And 2
- WO #353856-07; Install 2FF-07-02C Heat Trace Cable On RS-SA-003 And Test  
- Drawing 325073; Facade Freeze Protection Control Panel 1FFCP-02B; Secondary Distribution
- WO #366472; 2VNTB-04802A Damper Not Fully Closing  
  Breaker Panelboard 1FFDP-02-5; Unit 1
- Drawing 019193; Electrical Layout Facade Area E-142; Unit 1  
- Generic Letter 88-20; Supplement 5; Individual Plant Examination Of External Events For
- Drawing 55805; Wiring Diagram Heat Tracing Panel "AH"; Auxiliary Building; Units 1 And 2  
  Severe Accident Vulnerabilities
- Drawing 325073; Facade Freeze Protection Control Panel 1FFCP-02B; Secondary Distribution  
1R04 Equipment Alignment
Breaker Panelboard 1FFDP-02-5; Unit 1  
- 2-SOP-RH-002; Residual Heat Removal System Operation; Revision 3
- Generic Letter 88-20; Supplement 5; Individual Plant Examination Of External Events For  
- CL 7A; Safety Injection System Checklist Unit 2; Revision 30
Severe Accident Vulnerabilities  
- CL 7B; Safety Injection System Checklist Unit 2; Revision 27
1R04 Equipment Alignment  
- IT 04F; 2P-10A LHSI Pump Profile Test Mode 6 High Cavity Water Level Unit 2; Revision 4
- 2-SOP-RH-002; Residual Heat Removal System Operation; Revision 3  
- O-TS-EP-001; Weekly Power Availability Verification; Revision 11
- CL 7A; Safety Injection System Checklist Unit 2; Revision 30  
- OP 7A; Placing Residual Heat Removal System In Operation; Revision 45
- CL 7B; Safety Injection System Checklist Unit 2; Revision 27  
- Drawing ISI-2122; Residual Heat Removal Suction From Loop "A"; Unit 2
- IT 04F; 2P-10A LHSI Pump Profile Test Mode 6 High Cavity Water Level Unit 2; Revision 4  
- Drawing ISI-2123; Residual Heat Removal Suction Header; Unit 2
- O-TS-EP-001; Weekly Power Availability Verification; Revision 11  
- Drawing ISI-2125; Residual Heat Removal To Loop "B"; Unit 2
- OP 7A; Placing Residual Heat Removal System In Operation; Revision 45  
- Drawing ISI-2204; Residual Heat Removal Heat Exchangers HX-11A And HX-11B; Unit 2
- Drawing ISI-2122; Residual Heat Removal Suction From Loop "A"; Unit 2  
- Drawing ISI-2228; Residual Heat Removal Pump Discharge; Unit 2
- Drawing ISI-2123; Residual Heat Removal Suction Header; Unit 2  
- Drawing ISI-2231; Residual Heat Removal Heat Exchanger Bypass; Unit 2
- Drawing ISI-2125; Residual Heat Removal To Loop "B"; Unit 2  
- Drawing ISI-PRI-2131; Residual Heat Removal To RPV; Unit 2
- Drawing ISI-2204; Residual Heat Removal Heat Exchangers HX-11A And HX-11B; Unit 2  
- Valve And Component Map; Pipeway 3; EL 8" PAB; Revision 0
- Drawing ISI-2228; Residual Heat Removal Pump Discharge; Unit 2  
- Valve And Component Map; Unit 2 RHR Heat Exchanger Cubicle; EL 5' PAB; Revision 4
- Drawing ISI-2231; Residual Heat Removal Heat Exchanger Bypass; Unit 2  
- Valve And Component Map; Pipeway 3; Hallway Outside; EL 8' PAB; Revision 2
- Drawing ISI-PRI-2131; Residual Heat Removal To RPV; Unit 2  
- Valve And Component Map; U2C - 46'; Revision 2
- Valve And Component Map; Pipeway 3; EL 8" PAB; Revision 0  
- Valve And Component Map; Unit 2 Containment; 10' And 21' Elevation; Revision 2
- Valve And Component Map; Unit 2 RHR Heat Exchanger Cubicle; EL 5' PAB; Revision 4  
- Valve And Component Map; U2 A S/G Handhole Level; Area 2C-8; Revision 2
- Valve And Component Map; Pipeway 3; Hallway Outside; EL 8' PAB; Revision 2  
- Valve And Component Map; Unit 2 Containment "A" 10' Platform; Revision 3
- Valve And Component Map; U2C - 46'; Revision 2  
1R05 Fire Protection
- Valve And Component Map; Unit 2 Containment; 10' And 21' Elevation; Revision 2  
- FEP 4.0; Fire Emergency Plan; Revision 5
- Valve And Component Map; U2 A S/G Handhole Level; Area 2C-8; Revision 2  
- FEP 4.20; Site; Revision 7
- Valve And Component Map; Unit 2 Containment "A" 10' Platform; Revision 3  
- FEP 4.26; North Service Building; Revision 3
1R05 Fire Protection  
- FHAR FZ245; Fire Area A01-E; Electrical Equipment Room - Unit 1; Fire Zone Data
- FEP 4.0; Fire Emergency Plan; Revision 5  
- FHAR FZ775; Fire Area A71; G-04 Diesel Room; Fire Zone Data
- FEP 4.20; Site; Revision 7  
- FOP 1.1; Brigade Training; Revision 9
- FEP 4.26; North Service Building; Revision 3  
- NP 1.9.14; Fire Protection Organization; Revision 10
- FHAR FZ245; Fire Area A01-E; Electrical Equipment Room - Unit 1; Fire Zone Data  
- PC 74; Conducting And Evaluating Fire Drills; Revision 10
- FHAR FZ775; Fire Area A71; G-04 Diesel Room; Fire Zone Data  
- Drawing 290590; Fire Protection For Turbine Building, Auxiliary Building And Containment;
- FOP 1.1; Brigade Training; Revision 9  
  Elevation 44' - 0"
- NP 1.9.14; Fire Protection Organization; Revision 10  
- Shift Staffing Report; Station Log; Mid-Shift; December 10, 2009
- PC 74; Conducting And Evaluating Fire Drills; Revision 10  
                                                4                                  Attachment
- Drawing 290590; Fire Protection For Turbine Building, Auxiliary Building And Containment;  
Elevation 44' - 0"
- Shift Staffing Report; Station Log; Mid-Shift; December 10, 2009  


1R06 Flood Protection Measures
- AOP-9A; Service Water System Malfunction; Revision 24
5
- FSAR Appendix A.7; Plant Internal Flooding
Attachment
- NP 8.4.17; PBNP Flooding Barrier Control; Revision 10
1R06 Flood Protection Measures  
1R08 Inservice Inspection Activities
- AOP-9A; Service Water System Malfunction; Revision 24  
- AR 01142750; U2R30 Inservice Inspection
- FSAR Appendix A.7; Plant Internal Flooding  
- AR 01160164; Delays In RPV Examinations
- NP 8.4.17; PBNP Flooding Barrier Control; Revision 10  
- AR 01153595; EPRI Issued Document For Dissimilar Metal Weld UT Exams
1R08 Inservice Inspection Activities  
- AR 01144460; WCAP-15666-A (Reactor Coolant Pump Flywheel Examinations)
- AR 01142750; U2R30 Inservice Inspection  
- AR 01125657; OE26445 - Nondestructive Examination Results Affect Core
- AR 01160164; Delays In RPV Examinations  
- NDE-163; Manual Ultrasonic Examination Of Ferritic Pressure Vessel Welds Greater Than 2
- AR 01153595; EPRI Issued Document For Dissimilar Metal Weld UT Exams  
  Inches In Thickness; Revision 14
- AR 01144460; WCAP-15666-A (Reactor Coolant Pump Flywheel Examinations)  
- NDE-109; Manual Ultrasonic Examination Using Longitudinal-Wave Straight-Beam
- AR 01125657; OE26445 - Nondestructive Examination Results Affect Core  
  Techniques; Revision 8
- NDE-163; Manual Ultrasonic Examination Of Ferritic Pressure Vessel Welds Greater Than 2  
- NDE-171; Manual Ultrasonic Examination Of Nozzle Inside Radius Sections; Revision 13
Inches In Thickness; Revision 14  
- NDE-451; Visible Dye Penetrant Examination Temperature Applications 45°F TO 125°F;
- NDE-109; Manual Ultrasonic Examination Using Longitudinal-Wave Straight-Beam  
  Revision 25
Techniques; Revision 8  
- NDE-753; Visual Examination (VT-2) Leakage Detection Of Nuclear Power Plant Components;
- NDE-171; Manual Ultrasonic Examination Of Nozzle Inside Radius Sections; Revision 13  
  Revision 15
- NDE-451; Visible Dye Penetrant Examination Temperature Applications 45°F TO 125°F;  
- NDE-757; Visual Examination For Leakage Of Pressure Vessel Penetrations; Revision 7
Revision 25  
- AM 3-31; Alloy 600 Management Program; Revision 4
- NDE-753; Visual Examination (VT-2) Leakage Detection Of Nuclear Power Plant Components;  
- Work Order Package 00352519; Replacement Of An ASME Section III, Class 1, RCS
Revision 15  
   To P-10A/B Residual Heat Removal Pump Suction Header Drain Valve 2RH-D-9
- NDE-757; Visual Examination For Leakage Of Pressure Vessel Penetrations; Revision 7  
- Work Order Package 00352831; Replacement Of An ASME Section III, Class 1, Excess
- AM 3-31; Alloy 600 Management Program; Revision 4  
  Letdown Heat Exchanger 2HX-4 Outlet Drain Valve 2CV-D-11
- Work Order Package 00352519; Replacement Of An ASME Section III, Class 1, RCS  
1R11 Licensed Operator Requalification Program
   To P-10A/B Residual Heat Removal Pump Suction Header Drain Valve 2RH-D-9  
- OP 1B; Reactor Startup; Revision 60
- Work Order Package 00352831; Replacement Of An ASME Section III, Class 1, Excess  
- OP 1C; Startup To Power Operation Unit 2; Revision 15
Letdown Heat Exchanger 2HX-4 Outlet Drain Valve 2CV-D-11
- Results Of Licensed Operator Annual Operating Tests; 2009
1R11 Licensed Operator Requalification Program  
1R12 Maintenance Rule Implementation
- OP 1B; Reactor Startup; Revision 60  
- AM 3-4; Implementation Of The Maintenance Rule At PBNP; Revision 7
- OP 1C; Startup To Power Operation Unit 2; Revision 15  
- AR 01157305; Delayed Inspection Raises GL 89-13 Program And CCW Questions
- Results Of Licensed Operator Annual Operating Tests; 2009  
- AR 01159196; 2HX-015D Containment Fan Coolers Blocked With Mussels
1R12 Maintenance Rule Implementation  
- NAP-407; Equipment Reliability; Revision 5
- AM 3-4; Implementation Of The Maintenance Rule At PBNP; Revision 7
- NP 7.7.4; Scope And Risk Significant Determination For The Maintenance Rule; Revision 17
- AR 01157305; Delayed Inspection Raises GL 89-13 Program And CCW Questions  
- NP 7.7.5; Maintenance Rule Monitoring; Revision 21
- AR 01159196; 2HX-015D Containment Fan Coolers Blocked With Mussels  
- NP 7.7.7; Maintenance Rule Periodic Evaluation; Revision 4
- NAP-407; Equipment Reliability; Revision 5  
- SEM 4.2; Component Maintenance Program Guideline; Revision 4
- NP 7.7.4; Scope And Risk Significant Determination For The Maintenance Rule; Revision 17  
- Evaluation Of Exceeding The Assumed Value For Partially Blocked Flowpaths For The
- NP 7.7.5; Maintenance Rule Monitoring; Revision 21  
   Inspection Of Containment Fan Cooler 2HX-015A (EC14792)
- NP 7.7.7; Maintenance Rule Periodic Evaluation; Revision 4  
- Evaluation Of Exceeding The Assumed Value For Partially Blocked Flowpaths For The
- SEM 4.2; Component Maintenance Program Guideline; Revision 4  
   Inspection Of Containment Fan Cooler 2HX-015C And 2HX-015D (EC14793)
- Evaluation Of Exceeding The Assumed Value For Partially Blocked Flowpaths For The  
- Point Beach GT System Corrective Action Plan; Revision 0 and 1
   Inspection Of Containment Fan Cooler 2HX-015A (EC14792)  
- Point Beach SE-0401 Action Tracking Data; Gas Turbine AR/CAPs
- Evaluation Of Exceeding The Assumed Value For Partially Blocked Flowpaths For The  
                                            5                                  Attachment
   Inspection Of Containment Fan Cooler 2HX-015C And 2HX-015D (EC14793)  
- Point Beach GT System Corrective Action Plan; Revision 0 and 1  
- Point Beach SE-0401 Action Tracking Data; Gas Turbine AR/CAPs  


- Point Beach Gas Turbine System Health Report - Third Quarter 2009
- Point Beach Third Quarter System Matrix; July 1 - September 30, 2009
6
- Point Beach Fourth Quarter System Matrix; October 1 - December 31, 2009
Attachment
- Point Beach Smart System Status Report; Gas Turbine System; December 15, 2007
- Point Beach Gas Turbine System Health Report - Third Quarter 2009  
- Point Beach Smart System Status Report; Gas Turbine System; January 17, 2008
- Point Beach Third Quarter System Matrix; July 1 - September 30, 2009  
- Point Beach Smart System Status Report; Gas Turbine System; February 28, 2008
- Point Beach Fourth Quarter System Matrix; October 1 - December 31, 2009  
- Point Beach Smart System Status Report; Gas Turbine System; May 2, 2008
- Point Beach Smart System Status Report; Gas Turbine System; December 15, 2007  
- Point Beach Smart System Status Report; Gas Turbine System; August 1, 2008
- Point Beach Smart System Status Report; Gas Turbine System; January 17, 2008  
- Point Beach Smart System Status Report; Gas Turbine System; January 1, 2009
- Point Beach Smart System Status Report; Gas Turbine System; February 28, 2008  
- Point Beach Smart System Status Report; Gas Turbine System; February 23, 2009
- Point Beach Smart System Status Report; Gas Turbine System; May 2, 2008  
- Point Beach Nuclear Plant Maintenance Rule (a)(1) Action Plan Timeline Data
- Point Beach Smart System Status Report; Gas Turbine System; August 1, 2008  
- Point Beach Nuclear Plant Maintenance Rule Unavailability Data Sheet;
- Point Beach Smart System Status Report; Gas Turbine System; January 1, 2009  
   June 1, 2009 - November 1, 2009
- Point Beach Smart System Status Report; Gas Turbine System; February 23, 2009  
- GL 89-13 Program Document; Revision 8
- Point Beach Nuclear Plant Maintenance Rule (a)(1) Action Plan Timeline Data
- Procedure AM 3-19; Biofouling Control Program; Revision 4
- Point Beach Nuclear Plant Maintenance Rule Unavailability Data Sheet;  
- Procedure OI 155; Chemical Treatment of Service Water for Mussels; Revision 27
   June 1, 2009 - November 1, 2009  
- Calculation 2002-0008; CCW HX Plugging Limit; Revision 3
- GL 89-13 Program Document; Revision 8  
- AR 01158115; Unexpected TSAC Entry due to low accident cooler SW flow
- Procedure AM 3-19; Biofouling Control Program; Revision 4  
- AR 01158344; 2HX-12D CC HX Found to be Approximately 66% blocked
- Procedure OI 155; Chemical Treatment of Service Water for Mussels; Revision 27  
- AR 01159196; 2HS-1015D Containment Fan Cooler Blocked with Mussels
- Calculation 2002-0008; CCW HX Plugging Limit; Revision 3  
- AR 01159293; Significant Number of Blocked Tubes on 2HX-15C CFC
- AR 01158115; Unexpected TSAC Entry due to low accident cooler SW flow  
- AR 01159787; HX-12C CCW HX Exceeds Allowed Blocked Tubes
- AR 01158344; 2HX-12D CC HX Found to be Approximately 66% blocked
- AR 01159890; Tubes Blocked in 2HX-12D
- AR 01159196; 2HS-1015D Containment Fan Cooler Blocked with Mussels  
- AR 01160350; U2 "A CFC Exceeded Plugging Limits per Calculation 2002-0003
- AR 01159293; Significant Number of Blocked Tubes on 2HX-15C CFC  
- EC14794; Evaluation of the Effect of the Blocked Flowpaths Found during the Inspection of
- AR 01159787; HX-12C CCW HX Exceeds Allowed Blocked Tubes  
  HX-12C and 2HX-12D; December 10, 2009
- AR 01159890; Tubes Blocked in 2HX-12D  
- HX-12C BIO/SILT Fouling Inspection Program Form, Inspection dated October 27, 2009
- AR 01160350; U2 "A CFC Exceeded Plugging Limits per Calculation 2002-0003  
- HX-12D BIO/SILT Fouling Inspection Program Form, Inspection dated October 28, 2009
- EC14794; Evaluation of the Effect of the Blocked Flowpaths Found during the Inspection of  
- HX-15C-6 BIO/SILT Fouling Inspection Program Form, Inspection dated October 22, 2009
HX-12C and 2HX-12D; December 10, 2009  
1R13 Maintenance Risk Assessments and Emergent Work Control
- HX-12C BIO/SILT Fouling Inspection Program Form, Inspection dated October 27, 2009  
- AR 01161450; Availability Of AFW Piping For Mode 5 Steam Generator Availability
- HX-12D BIO/SILT Fouling Inspection Program Form, Inspection dated October 28, 2009  
- AR 01161450; Availability Of AFW Piping For Mode 5 Steam Generator Availability
- HX-15C-6 BIO/SILT Fouling Inspection Program Form, Inspection dated October 22, 2009  
- IN 95-35; Degraded Ability Of Steam Generators To Remove Decay Heat By Natural
1R13 Maintenance Risk Assessments and Emergent Work Control  
   Circulation
- AR 01161450; Availability Of AFW Piping For Mode 5 Steam Generator Availability  
- NP 10.3.6; Shutdown Safety Review And Safety Assessment; Revision 30
- AR 01161450; Availability Of AFW Piping For Mode 5 Steam Generator Availability  
- Control Room Log Entries Report; November 15 - 17, 2009
- IN 95-35; Degraded Ability Of Steam Generators To Remove Decay Heat By Natural  
- Drawing 25494-200-M0K-0000-06061; Weld Map For FE-4036 Assembly
   Circulation  
- Drawing 342215; ISI Isometric Auxiliary Feedwater To Steam Generator "B"
- NP 10.3.6; Shutdown Safety Review And Safety Assessment; Revision 30  
- Drawing 342217; ISI Isometric Auxiliary Feedwater To Steam Generator "A"
- Control Room Log Entries Report; November 15 - 17, 2009  
1R15 Operability Evaluations
- Drawing 25494-200-M0K-0000-06061; Weld Map For FE-4036 Assembly  
- AR 01147224; Spent Fuel Pool Cooling Pump Was Rendered Non-Functional
- Drawing 342215; ISI Isometric Auxiliary Feedwater To Steam Generator "B"  
- AR 01148036; P-12B Spent Fuel Pool Pump's RV Not Indicative Of True Performance
- Drawing 342217; ISI Isometric Auxiliary Feedwater To Steam Generator "A"  
- AR 01156117; EPU Spent Fuel Pool Cooling Calculation Issues
1R15 Operability Evaluations  
- AR 01159196; 2HX-015D Containment Fan Coolers Blocked With Mussels
- AR 01147224; Spent Fuel Pool Cooling Pump Was Rendered Non-Functional  
- AR 01160033; Apparent SW Leak; Unit 2 CFC HX-015A1-A4 Coils
- AR 01148036; P-12B Spent Fuel Pool Pump's RV Not Indicative Of True Performance  
- AR 01161636; New AFW Line In Contact With SW Pipe
- AR 01156117; EPU Spent Fuel Pool Cooling Calculation Issues  
- AR 01160007; Evidence Of Leakage From HX15A1-4
- AR 01159196; 2HX-015D Containment Fan Coolers Blocked With Mussels  
                                              6                                  Attachment
- AR 01160033; Apparent SW Leak; Unit 2 CFC HX-015A1-A4 Coils  
- AR 01161636; New AFW Line In Contact With SW Pipe  
- AR 01160007; Evidence Of Leakage From HX15A1-4  


- AR 01160262; 1HX-15C CFC Flow Out Of Limit Low Per TS-33
- AR 01160350; U2 "A" CFC Exceeded Plugging Limits Per Calculation 2002-0003
7
- AR 01160443; Found Washer Between Gasket And Flange Face On 2HX-15A3
Attachment
- AR 01162022; Spent Fuel Pool Cooling System Incorrectly Classified
- AR 01160262; 1HX-15C CFC Flow Out Of Limit Low Per TS-33
- AR 1159784; Spent Fuel Pool Pump Suction Isolation Valve Stem Contacting Adjacent Pipe
- AR 01160350; U2 "A" CFC Exceeded Plugging Limits Per Calculation 2002-0003  
   Insulation
- AR 01160443; Found Washer Between Gasket And Flange Face On 2HX-15A3  
- AR 1160262; 1HX-15C CFC Flow Out Of Limit Low Per TS-33
- AR 01162022; Spent Fuel Pool Cooling System Incorrectly Classified  
- CL 5C; Spent Fuel Pool Cooling And Refueling Water Circulating Pump Normal Operation
- AR 1159784; Spent Fuel Pool Pump Suction Isolation Valve Stem Contacting Adjacent Pipe  
   Valve Lineup
   Insulation  
- DG-M09; Design Requirements For Piping Stress Analysis; Revision 2
- AR 1160262; 1HX-15C CFC Flow Out Of Limit Low Per TS-33  
- EN-AA-203-1001; Operability Determinations/Functionality Assessments; Revision 1
- CL 5C; Spent Fuel Pool Cooling And Refueling Water Circulating Pump Normal Operation  
- NP 8.4.10; Exclusion Of Foreign Material From Plant Components And Systems;
   Valve Lineup  
   Revisions 7 and 24
- DG-M09; Design Requirements For Piping Stress Analysis; Revision 2  
- TS 33; Containment Accident Recirculation Fan-Cooler Units (Monthly); Unit 1; Revision 31
- EN-AA-203-1001; Operability Determinations/Functionality Assessments; Revision 1  
- Causal Evaluation; 2SI-897B Failed To Operate (AR 1158812, AR1158797/WO 379810);
- NP 8.4.10; Exclusion Of Foreign Material From Plant Components And Systems;  
   October 22, 2009
   Revisions 7 and 24  
- Drawing 018993; Auxiliary Cooling System; Unit 1; Revision 44
- TS 33; Containment Accident Recirculation Fan-Cooler Units (Monthly); Unit 1; Revision 31  
- Drawing 018995; P&ID Service Water; Unit 1
- Causal Evaluation; 2SI-897B Failed To Operate (AR 1158812, AR1158797/WO 379810);  
- Point Beach Nuclear Plant A-46 Final Report; Introduction And Seismic Verification
   October 22, 2009  
   Methodology; Revision 1
- Drawing 018993; Auxiliary Cooling System; Unit 1; Revision 44  
- Point Beach Nuclear Plant A-46 Final Report; Appendix A; Seismic Design For Structures and
- Drawing 018995; P&ID Service Water; Unit 1  
   Equipment
- Point Beach Nuclear Plant A-46 Final Report; Introduction And Seismic Verification  
1R18 Plant Modifications
   Methodology; Revision 1  
- 07 Calculation 2009-0022; Air Entrainment for Containment Sump Screens; 2009
- Point Beach Nuclear Plant A-46 Final Report; Appendix A; Seismic Design For Structures and  
- AR 01122278; Safe Load Paths For Turbine Building Crane
   Equipment  
- AR 01145715; SLP 3 Revision 11 For Precautions Needed Over U2 Truck Bay
1R18 Plant Modifications  
- CA 0112278; Safe Load Paths For Turbine Building Crane
- 07 Calculation 2009-0022; Air Entrainment for Containment Sump Screens; 2009  
- 10 CFR 50.59/72.48 Screening For CA 0112278; Safe Load Paths For Turbine Building Crane
- AR 01122278; Safe Load Paths For Turbine Building Crane  
- AR 01159514; 5B FWTR Heater Contacted And Damaged Component
- AR 01145715; SLP 3 Revision 11 For Precautions Needed Over U2 Truck Bay  
- AR 01162492; ACE 01157505 Failed To Meet Minimum Requirements
- CA 0112278; Safe Load Paths For Turbine Building Crane  
- EC 11542; Unit 2 Main Generator Circuit Breaker Addition
- 10 CFR 50.59/72.48 Screening For CA 0112278; Safe Load Paths For Turbine Building Crane  
- 10 CFR 50.59 Evaluation of EC 11542; Unit 2 Main generator Circuit Breaker Addition
- AR 01159514; 5B FWTR Heater Contacted And Damaged Component  
- EC 12601; Additional Sump Strainer Modules - Unit 2; October 1, 2009
- AR 01162492; ACE 01157505 Failed To Meet Minimum Requirements  
- EC 13601; GSI-191 RCP, S/G, and RCS Loops Piping Insulation Replacement - Unit 2;
- EC 11542; Unit 2 Main Generator Circuit Breaker Addition  
  February 11, 2008
- 10 CFR 50.59 Evaluation of EC 11542; Unit 2 Main generator Circuit Breaker Addition  
- EC 14790; Validation of SSCs above the Unit 1 Sump B Suction Strainers; November 15,
- EC 12601; Additional Sump Strainer Modules - Unit 2; October 1, 2009  
  2009
- EC 13601; GSI-191 RCP, S/G, and RCS Loops Piping Insulation Replacement - Unit 2;  
- EN-AA-203-1001; Operability Determinations/Functionality Assessments; October 8, 2009
February 11, 2008  
- FSAR Appendix A.3; Control Of Heavy Loads
- EC 14790; Validation of SSCs above the Unit 1 Sump B Suction Strainers; November 15,  
- MDB 3.2.5 1B30; 480 V AC Motor Control Centers; Unit 1; Revision 2
2009  
- MDB 3.2.6 2B30; 480 V AC Motor Control Centers; Unit 2; Revision 1
- EN-AA-203-1001; Operability Determinations/Functionality Assessments; October 8, 2009  
- OI 35B; Electrical Equipment General Information; Revision 14
- FSAR Appendix A.3; Control Of Heavy Loads  
- PASS 002452; Electrical Raceways - Unit 2 Containment 8ft; November 4, 2009
- MDB 3.2.5 1B30; 480 V AC Motor Control Centers; Unit 1; Revision 2  
- PBNP Engineering Planning And Management Cable Schedule Data; Train "A" Cables
- MDB 3.2.6 2B30; 480 V AC Motor Control Centers; Unit 2; Revision 1  
- PBNP U2R30 Draft Schedule (Fall 2009); September 2, 2009
- OI 35B; Electrical Equipment General Information; Revision 14  
- PBNP U2R30 Production Schedule; 72-Hour Look Ahead; October 18, 2009
- PASS 002452; Electrical Raceways - Unit 2 Containment 8ft; November 4, 2009  
- SCR 2009-0127-01; GSI-191 RCP, S/G, and RCS Loops Piping Insulation Replacement -
- PBNP Engineering Planning And Management Cable Schedule Data; Train "A" Cables  
   Unit 2; September 8, 2009
- PBNP U2R30 Draft Schedule (Fall 2009); September 2, 2009  
- SFS-PB2-GA-00; Sure-Flow Strainer Recirc Sump System Layout; February 18, 2009
- PBNP U2R30 Production Schedule; 72-Hour Look Ahead; October 18, 2009  
                                              7                                      Attachment
- SCR 2009-0127-01; GSI-191 RCP, S/G, and RCS Loops Piping Insulation Replacement -
   Unit 2; September 8, 2009  
- SFS-PB2-GA-00; Sure-Flow Strainer Recirc Sump System Layout; February 18, 2009  


- SFS-PB2-GA-01; Sure-Flow Strainer General Notes; March 3, 2009
- SLP 3; Turbine Building Main Crane; Revisions 11 And 12-Draft A
8
- Bechtel Power Corporation Correspondence; Interim Load Paths For Safety-Related Handling
Attachment
   Devices; October 8, 1981
- SFS-PB2-GA-01; Sure-Flow Strainer General Notes; March 3, 2009  
- Drawing 19739; Lighting Schedule Panel 7L; Revision 22
- SLP 3; Turbine Building Main Crane; Revisions 11 And 12-Draft A  
- Drawing 080034; P&ID Service Water; Unit 1; Revision 65
- Bechtel Power Corporation Correspondence; Interim Load Paths For Safety-Related Handling  
- Drawing 6704-E-151001; Diesel Generator Building Yard Area Grading Plan; Revision 4
   Devices; October 8, 1981  
- Drawing 6704-E-353403; Yard Area Diesel Generator Duct Bank Plan; Revision 5
- Drawing 19739; Lighting Schedule Panel 7L; Revision 22  
- Drawing 82607-G1.0; Old FWH 5A And 5B Removal; Revision 1
- Drawing 080034; P&ID Service Water; Unit 1; Revision 65  
- Drawing M-2007; Equipment Location - Plan; Ground Floor North; Revision 19
- Drawing 6704-E-151001; Diesel Generator Building Yard Area Grading Plan; Revision 4  
- Hatch Area Study Design; Truck Bay, Gantry Track, Door Position And Opening, A/B Train
- Drawing 6704-E-353403; Yard Area Diesel Generator Duct Bank Plan; Revision 5  
   Duct Banks
- Drawing 82607-G1.0; Old FWH 5A And 5B Removal; Revision 1  
- Hatch Area Study With FWHTR Design; Truck Bay, Gantry Track, Door Position And Opening,
- Drawing M-2007; Equipment Location - Plan; Ground Floor North; Revision 19  
   A/B Train Duct Banks Feedwater Heater With Plates
- Hatch Area Study Design; Truck Bay, Gantry Track, Door Position And Opening, A/B Train  
- Hatch Area Study With Plates Design; Truck Bay, Gantry Track, Door Position And Opening,
   Duct Banks  
   A/B Train Duct Banks With Plates
- Hatch Area Study With FWHTR Design; Truck Bay, Gantry Track, Door Position And Opening,  
1R19 Post-Maintenance Testing
   A/B Train Duct Banks Feedwater Heater With Plates  
- AR 01159648; 2P-010B, Residual Heat Removal Pump Oiler Level Consumption
- Hatch Area Study With Plates Design; Truck Bay, Gantry Track, Door Position And Opening,  
- AR 01160385; Bechtel Identification Of Precursors To EPC Contract
   A/B Train Duct Banks With Plates  
- AR 01160661; Failed Radiographs On Welds For EC11683
1R19 Post-Maintenance Testing  
- AR 01161009; Failure Investigation Process Established Due To Repetitive Failure During
- AR 01159648; 2P-010B, Residual Heat Removal Pump Oiler Level Consumption  
   Radiographic Testing Of AFW Welds Associated With EC 133400
- AR 01160385; Bechtel Identification Of Precursors To EPC Contract  
- AR 01161191; Bechtel Corrective Action Report Not Written As Required
- AR 01160661; Failed Radiographs On Welds For EC11683  
- AR 01159839; Some Vent Valves Not Identified On Isometric Drawings (NRC-Identified)
- AR 01161009; Failure Investigation Process Established Due To Repetitive Failure During  
- AR 01159862; Acceptance Criteria For Gas Voids May Be Incomplete (NRC-Identified)
   Radiographic Testing Of AFW Welds Associated With EC 133400  
- AR 01159937; Sump Strainer Ii/I Seismic Documentation Incomplete (NRC-Identified)
- AR 01161191; Bechtel Corrective Action Report Not Written As Required  
- AR 01163219; Lack Of Documentation To Support A Decision Of 2/1 Acceptability
- AR 01159839; Some Vent Valves Not Identified On Isometric Drawings (NRC-Identified)  
  (NRC-Identified)
- AR 01159862; Acceptance Criteria For Gas Voids May Be Incomplete (NRC-Identified)  
- AR 01160941; No Requirement To Document Seismic II/I Evaluations; (NRC-Identified)
- AR 01159937; Sump Strainer Ii/I Seismic Documentation Incomplete (NRC-Identified)  
- AR 01158870; Found Badly Burned Contacts On 2B52-429K For Compressor K-4B
- AR 01163219; Lack Of Documentation To Support A Decision Of 2/1 Acceptability  
- AR 01159029; G-02 Foreign Material
(NRC-Identified)  
- AR 01159056; Found G-02 Emergency Diesel Generator Start Lockout Relay 2 Out Of
- AR 01160941; No Requirement To Document Seismic II/I Evaluations; (NRC-Identified)  
   Specification
- AR 01158870; Found Badly Burned Contacts On 2B52-429K For Compressor K-4B  
- AR 01159161; 40 T Relay In G-02 Found Out Of Specification
- AR 01159029; G-02 Foreign Material  
- AR 01159187; Mis-Communication During Work Activity
- AR 01159056; Found G-02 Emergency Diesel Generator Start Lockout Relay 2 Out Of  
- AR 01159410; Z-013 Main Hoist Has A Pinched Cable
   Specification  
- AR 01159721; Oil Addition To 2P-10B RHR Pump
- AR 01159161; 40 T Relay In G-02 Found Out Of Specification  
- AR 01159843; Thermal Overloads Found Tripped On 2B52-329K
- AR 01159187; Mis-Communication During Work Activity  
- AR 01159845; Minor Procedural Issues Encountered During G-02 PMT
- AR 01159410; Z-013 Main Hoist Has A Pinched Cable  
- AR 01159960; 2P-010B Oiler Adjustment Mechanism Setup Improperly
- AR 01159721; Oil Addition To 2P-10B RHR Pump  
- AR 01160179; 2P-10A RHR Pump Oiler May Be Incorrectly Installed
- AR 01159843; Thermal Overloads Found Tripped On 2B52-329K  
- AR 01160366; Low Flow Indication In OI 136A RHR "A" Train F & V
- AR 01159845; Minor Procedural Issues Encountered During G-02 PMT  
- AR 01160551; Inconsistent RHR Flow Limitations In Various Procedures
- AR 01159960; 2P-010B Oiler Adjustment Mechanism Setup Improperly  
- AR 01160557; Discrepancies Found During NRC Observed IT-04A RHR Test
- AR 01160179; 2P-10A RHR Pump Oiler May Be Incorrectly Installed  
- AR 01160749; SLP-1 And -2 Conflict With OSHA Required Crane Checks
- AR 01160366; Low Flow Indication In OI 136A RHR "A" Train F & V  
- AR 01161191; No Corrective Action Report Has Been Written To Document Trend Of Failed
- AR 01160551; Inconsistent RHR Flow Limitations In Various Procedures  
   Welds
- AR 01160557; Discrepancies Found During NRC Observed IT-04A RHR Test  
- AR 01161192; Contrary to Requirement A 3-Inch Elbow Between Welds 44Q And 44M On
- AR 01160749; SLP-1 And -2 Conflict With OSHA Required Crane Checks  
   The Auxiliary Feed Water Project Was Cut Out Due To Being Deficient
- AR 01161191; No Corrective Action Report Has Been Written To Document Trend Of Failed  
                                            8                                    Attachment
   Welds  
- AR 01161192; Contrary to Requirement A 3-Inch Elbow Between Welds 44Q And 44M On  
   The Auxiliary Feed Water Project Was Cut Out Due To Being Deficient  


- AR 01161222; Site Evaluation Of NRC Information Notice 2009-20
- AR 01161691; Main generator Rotor(s) Weight Exceeds TB Crane (Z-14) Capacity
9
- AR 01161694; New Generator Rotor Weight Exceeds TB Crane (Z-14) Capacity
Attachment
- AR 01161706; ASME B30.2 Code Year For Wire Rope Inspections
- AR 01161222; Site Evaluation Of NRC Information Notice 2009-20  
- AR 01161946; ACE 1160527 Not Accepted In A timely Manner
- AR 01161691; Main generator Rotor(s) Weight Exceeds TB Crane (Z-14) Capacity  
- AR 01162048; Load Block Leveler And White Substance On Wire Rope On Z-015
- AR 01161694; New Generator Rotor Weight Exceeds TB Crane (Z-14) Capacity  
- AR 01162940; Work Orders Not Yet Completed From RCE
- AR 01161706; ASME B30.2 Code Year For Wire Rope Inspections  
- IT 04A; RHR Pump And Valve Tests In DHR Mode (Cold Shutdown); Unit 2; Revision 26
- AR 01161946; ACE 1160527 Not Accepted In A timely Manner  
- PI-AA-100-1002; Guideline For Failure Investigation Process; Revision 0
- AR 01162048; Load Block Leveler And White Substance On Wire Rope On Z-015  
- 2-SOP-RH-002; Residual Heat Removal System Operation; Revision 3
- AR 01162940; Work Orders Not Yet Completed From RCE  
- TS 3.7.5; Auxiliary Feedwater
- IT 04A; RHR Pump And Valve Tests In DHR Mode (Cold Shutdown); Unit 2; Revision 26  
- TS 82; Emergency Diesel Generator G-02 Monthly; Revision 77
- PI-AA-100-1002; Guideline For Failure Investigation Process; Revision 0  
- WO 376979; Replace Wire Rope On the Polar Crane; Unit 2
- 2-SOP-RH-002; Residual Heat Removal System Operation; Revision 3  
- Drawing 25494-200-M0K-0000-06061; Weld Map For FE-4036 Assembly; Revision 4
- TS 3.7.5; Auxiliary Feedwater  
- Drawing 25494-200-M0K-0000-06062; Weld Map For 2FE-04036 Spool; Revision 1
- TS 82; Emergency Diesel Generator G-02 Monthly; Revision 77  
- Drawing 25494-200-M0K-0000-06063; Weld Map For 2FE-4037 Assembly; Revision 6
- WO 376979; Replace Wire Rope On the Polar Crane; Unit 2  
- Drawing 25494-200-M0K-0000-06064; Weld Map For 2FE-4037 Spool; Revision 1
- Drawing 25494-200-M0K-0000-06061; Weld Map For FE-4036 Assembly; Revision 4  
- Master Weld Log - Job No. 25494; Weld Map For 2FE-4037 Spool
- Drawing 25494-200-M0K-0000-06062; Weld Map For 2FE-04036 Spool; Revision 1  
- Point Beach Daily Quality Summary; November 12, 2009
- Drawing 25494-200-M0K-0000-06063; Weld Map For 2FE-4037 Assembly; Revision 6  
- Point Beach U2R30 Outage Schedule; Polar Crane Cable Repair Data; October 25-26, 2009
- Drawing 25494-200-M0K-0000-06064; Weld Map For 2FE-4037 Spool; Revision 1  
- Polar Crane 2Z-013 Estimated Wire Rope Stretch Data
- Master Weld Log - Job No. 25494; Weld Map For 2FE-4037 Spool  
- Trico Manufacturing Corp; Technical Information Sheet; Effects Of Aeration On Constant Level
- Point Beach Daily Quality Summary; November 12, 2009  
   Oilers
- Point Beach U2R30 Outage Schedule; Polar Crane Cable Repair Data; October 25-26, 2009  
- Trico Manufacturing Corp; Technical Information Sheet; Affects Of Air Movement On
- Polar Crane 2Z-013 Estimated Wire Rope Stretch Data  
   Opto-Matic Oilers
- Trico Manufacturing Corp; Technical Information Sheet; Effects Of Aeration On Constant Level  
- Trico Manufacturing Corp; Technical Information Sheet; Glass, LS, Or SS Opto-Matic Oilers
   Oilers  
   Instructions Before Installing
- Trico Manufacturing Corp; Technical Information Sheet; Affects Of Air Movement On  
- Trico Manufacturing Corp; Technical Information Sheet; Opto-Matic Installation
   Opto-Matic Oilers  
- Trico Manufacturing Corp; Technical Information Sheet; Preventing Excessive Lubrication In
- Trico Manufacturing Corp; Technical Information Sheet; Glass, LS, Or SS Opto-Matic Oilers  
   Oil Sump Applications
   Instructions Before Installing  
- Weld Failure Casual Evaluation; Aux Feed/Containment Spray Weld Failures;
- Trico Manufacturing Corp; Technical Information Sheet; Opto-Matic Installation  
   November 14, 2009
- Trico Manufacturing Corp; Technical Information Sheet; Preventing Excessive Lubrication In  
1R20 Refueling And Other Outage Activities
   Oil Sump Applications  
- AOP-2B; Unit 2; Feedwater System Malfunction; Revision 15
- Weld Failure Casual Evaluation; Aux Feed/Containment Spray Weld Failures;  
- AR 01158914; Reactor Vessel Level Indication Wide Range Calculations On Hold
   November 14, 2009  
- AR 01160451; Add Transmitter Valving To I&C Pre-Outage Training
1R20 Refueling And Other Outage Activities  
- AR 01161576; Unit 2 Reactor Heat Removal Components Will Exceed 125 Percent
- AOP-2B; Unit 2; Feedwater System Malfunction; Revision 15  
- AR 01161998; Revise 535A To Better Document Full Stroke Manual Exercise Of 2RH-715C
- AR 01158914; Reactor Vessel Level Indication Wide Range Calculations On Hold  
- AR 01162196; Inservice Testing Program Acceptance Criteria
- AR 01160451; Add Transmitter Valving To I&C Pre-Outage Training  
- AR 01162379; Unit 2, 2CC-738A Valve Did Not Go Full Shut
- AR 01161576; Unit 2 Reactor Heat Removal Components Will Exceed 125 Percent  
- ASTM Designation; A 193/A 193M-93a; Standard Specification For Alloy-Steel And Stainless
- AR 01161998; Revise 535A To Better Document Full Stroke Manual Exercise Of 2RH-715C  
   Steel Bolting Materials For High-Temperature Service
- AR 01162196; Inservice Testing Program Acceptance Criteria  
- ASTM Designation; B 16/B 16M-00; Standard Specification For Free-Cutting Brass Rod, Bar
- AR 01162379; Unit 2, 2CC-738A Valve Did Not Go Full Shut  
   And Shapes For Use In Screw Machines-EC 14895; 2RH-716A - Yoke Bushing Nut Bolt
- ASTM Designation; A 193/A 193M-93a; Standard Specification For Alloy-Steel And Stainless  
   Installation
   Steel Bolting Materials For High-Temperature Service  
- AR 01159071; Unable To Complete 21CP 04.024 Due To Mode Change
- ASTM Designation; B 16/B 16M-00; Standard Specification For Free-Cutting Brass Rod, Bar  
- AR 01159076; Unexpected Unit 2 Reactor Vessel High Alarm
   And Shapes For Use In Screw Machines-EC 14895; 2RH-716A - Yoke Bushing Nut Bolt  
- AR 01161058; PMT for RC-537 Not Performed According To Work Order Task
   Installation  
- AR 01161630; Cut Reinforcing Bar In AFW Pump Room Wall
- AR 01159071; Unable To Complete 21CP 04.024 Due To Mode Change  
                                            9                                    Attachment
- AR 01159076; Unexpected Unit 2 Reactor Vessel High Alarm  
- AR 01161058; PMT for RC-537 Not Performed According To Work Order Task  
- AR 01161630; Cut Reinforcing Bar In AFW Pump Room Wall  


- AR 01161966; P-31B Discharge Elbow Support Degraded
- AR 01161994; Testing Of SG Atmospherics Prior To Mode 4
10
- AR 01162014; Issue With SG Atmospheric Testing In OP-1A
Attachment
- AR 01162073; Duct Tape On 2MS-02020 Yoke And Gland Follower
- AR 01161966; P-31B Discharge Elbow Support Degraded  
- AR 01162088; 2MS-2015 Atmospheric Dump Stroke Time Exceeded IST Limit
- AR 01161994; Testing Of SG Atmospherics Prior To Mode 4  
- AR 91162106; 2FD-2608 HX-22B MSR BTV Stuck In Mid Position
- AR 01162014; Issue With SG Atmospheric Testing In OP-1A  
- AR 01162110; 2AF-4006 Closed Light Continuity Not As Required
- AR 01162073; Duct Tape On 2MS-02020 Yoke And Gland Follower  
- AR 01162119; Lone Wire Laying On Floor Below Apron Section of 2C03
- AR 01162088; 2MS-2015 Atmospheric Dump Stroke Time Exceeded IST Limit  
- AR 01162139; MOB-276 Tripping
- AR 91162106; 2FD-2608 HX-22B MSR BTV Stuck In Mid Position  
- AR 01162146; Valve Contractor Missing Step Sign Offs
- AR 01162110; 2AF-4006 Closed Light Continuity Not As Required  
- AR 01162166; 2C-03 Control Board Indication Deficiencies
- AR 01162119; Lone Wire Laying On Floor Below Apron Section of 2C03  
- AR 01162202; Mode Change Hold Process Improvement Suggestions
- AR 01162139; MOB-276 Tripping  
- AR 01162223; U2 Purge Spool Pieces Restrict Access To Valves
- AR 01162146; Valve Contractor Missing Step Sign Offs  
- AR 01162253; BALCM - Dried Boric Acid Found On Packing Gland - 2SI-V-09
- AR 01162166; 2C-03 Control Board Indication Deficiencies  
- AR 01162316; Additive Valve Position Out-Of-Tolerance For GV 4
- AR 01162202; Mode Change Hold Process Improvement Suggestions  
- AR 01162353; Feed Pump Seal Inlet Valve Frozen/Doesn't Move
- AR 01162223; U2 Purge Spool Pieces Restrict Access To Valves  
- AR 01162379; Unit 2 2CC-738A Valve Did Not Go Full Shut
- AR 01162253; BALCM - Dried Boric Acid Found On Packing Gland - 2SI-V-09  
- AR 01163155; Ground Water Drain Line Dripping On U1F 6.5" Floor
- AR 01162316; Additive Valve Position Out-Of-Tolerance For GV 4  
- AR 01163605; Wrong Valves For Tubing And Valve Replacement For K-2b
- AR 01162353; Feed Pump Seal Inlet Valve Frozen/Doesn't Move  
- AR 01153633; 2Z-104B Needs Replacement
- AR 01162379; Unit 2 2CC-738A Valve Did Not Go Full Shut  
- CL 1B; Containment Barrier Checklist; Unit 2; Revision 58
- AR 01163155; Ground Water Drain Line Dripping On U1F 6.5" Floor  
- CL 2B; Mode 6 To Mode 5 Checklist; Revision 11
- AR 01163605; Wrong Valves For Tubing And Valve Replacement For K-2b  
- CL 2C; Mode 5 to Mode 4 Checklist; Revision 15
- AR 01153633; 2Z-104B Needs Replacement  
- CL 2E; Mode 3 To Mode 2 Checklist; Revision 16
- CL 1B; Containment Barrier Checklist; Unit 2; Revision 58  
- CL 20; Post Outage Containment Closeout Inspection; Revision 19
- CL 2B; Mode 6 To Mode 5 Checklist; Revision 11  
- CR 99-2241; Need To Evaluate Implementation Of The Service Water Model To Ensure
- CL 2C; Mode 5 to Mode 4 Checklist; Revision 15  
   Assumptions Are Valid
- CL 2E; Mode 3 To Mode 2 Checklist; Revision 16  
- EC 0014645; D-08 Battery Charger Temp Power From Alternate Source
- CL 20; Post Outage Containment Closeout Inspection; Revision 19  
- FP-E-MOD-02; Engineering Change Control; Revision 6
- CR 99-2241; Need To Evaluate Implementation Of The Service Water Model To Ensure  
- FP-E-RTC-02; Equipment Classification - Q List; Revision 4
   Assumptions Are Valid  
- IT 06; Containment Spray Pumps And Valves (Quarterly) Unit 2; Revision 61
- EC 0014645; D-08 Battery Charger Temp Power From Alternate Source  
- IT 45; Safety Injection Valves (Quarterly) Unit 2; Revision 51
- FP-E-MOD-02; Engineering Change Control; Revision 6  
- IT 45B; SI Valves (Shutdown) Unit 2; Revision 4
- FP-E-RTC-02; Equipment Classification - Q List; Revision 4  
- IT 395; Safety Injection Valves (Annual) Unit 2; Revision 12
- IT 06; Containment Spray Pumps And Valves (Quarterly) Unit 2; Revision 61  
- NP 4.2.19; Entry requirements Into Various Radiologically Controlled Areas; Revision 16
- IT 45; Safety Injection Valves (Quarterly) Unit 2; Revision 51  
- IWA-4000; Repair/Replacement Activities
- IT 45B; SI Valves (Shutdown) Unit 2; Revision 4  
- IWA-5000; System Pressure Tests
- IT 395; Safety Injection Valves (Annual) Unit 2; Revision 12  
- IWB-5000; System Pressure Tests
- NP 4.2.19; Entry requirements Into Various Radiologically Controlled Areas; Revision 16  
- MR 97-102; RC Piping Overpressurization Relief - Unit 1; Final Design Description;
- IWA-4000; Repair/Replacement Activities  
   October 22, 1997
- IWA-5000; System Pressure Tests  
- OI 53; Positioning Of The Fuel Transfer Cart; Revision 12
- IWB-5000; System Pressure Tests  
- OP 1A; Cold Shutdown To Hot Standby; Revision 99
- MR 97-102; RC Piping Overpressurization Relief - Unit 1; Final Design Description;  
- OP 1B; Reactor Startup; Revision 61
   October 22, 1997  
- OP 1C; Startup To Power Operation; Unit 2; Revision 16
- OI 53; Positioning Of The Fuel Transfer Cart; Revision 12  
- OP5A; Reactor Coolant Volume Control; Revision 42
- OP 1A; Cold Shutdown To Hot Standby; Revision 99  
- 10 CFR 50.99/72.48 Screening For MR 97-102; RC Piping Overpressurization Relief - Unit 1
- OP 1B; Reactor Startup; Revision 61  
- RESP 4.1; BOL Physics Tests; Revision 24
- OP 1C; Startup To Power Operation; Unit 2; Revision 16  
- TRHB 10.2; Primary Systems Descriptions: Reactor Coolant System; Revision 9
- OP5A; Reactor Coolant Volume Control; Revision 42  
- WO 00378956; 2RH-716A Yoke Bushing Nut Bolt Installation
- 10 CFR 50.99/72.48 Screening For MR 97-102; RC Piping Overpressurization Relief - Unit 1  
- 10 CFR 50.59/72.48 Screening of WO 00378956; 2RH-716A Yoke Bushing Nut Bolt
- RESP 4.1; BOL Physics Tests; Revision 24  
   Installation
- TRHB 10.2; Primary Systems Descriptions: Reactor Coolant System; Revision 9  
                                                10                                  Attachment
- WO 00378956; 2RH-716A Yoke Bushing Nut Bolt Installation  
- 10 CFR 50.59/72.48 Screening of WO 00378956; 2RH-716A Yoke Bushing Nut Bolt  
   Installation  


- 2-PT-RCS-1; Reactor Coolant System Pressure Test - Inside/Outside Containment; Unit 2;
   Revision 3
11
- 21CP 04.023-1; Reactor Vessel Level Outage Calibration; Revision 7
Attachment
- Calculation 2003-0057; Evaluation Of Service Water System Debris Transport To Auxiliary
- 2-PT-RCS-1; Reactor Coolant System Pressure Test - Inside/Outside Containment; Unit 2;  
   Feedwater
   Revision 3  
- Control Room Log Entries Data; October 19-20, 2009
- 21CP 04.023-1; Reactor Vessel Level Outage Calibration; Revision 7  
- Drawing 018941; Fuel Transfer Arrangement System 2224; Revision 6
- Calculation 2003-0057; Evaluation Of Service Water System Debris Transport To Auxiliary  
- Drawing 018977; Auxiliary Coolant System; Unit 2
   Feedwater  
- Drawing 152353; Auxiliary Cooling System; Residual Heat Exchanger; Discharge To
- Control Room Log Entries Data; October 19-20, 2009  
   Valve 720 To Loop B To Valve 742 To MOV 871 AC 601R-G; Unit 2
- Drawing 018941; Fuel Transfer Arrangement System 2224; Revision 6  
- Equipment Specification 677020; Fuel Transfer System; Revision 0
- Drawing 018977; Auxiliary Coolant System; Unit 2  
- NRC Generic Letter 88-17; Loss Of Decay Heat Removal 10 CFR 50.54(f); October 17, 1988
- Drawing 152353; Auxiliary Cooling System; Residual Heat Exchanger; Discharge To  
- Operations PCRA Backlog Scrub Data; December 23, 2009
   Valve 720 To Loop B To Valve 742 To MOV 871 AC 601R-G; Unit 2  
- Point Beach AT-0246 Outage Action Request Mode Change Restraints Data;
- Equipment Specification 677020; Fuel Transfer System; Revision 0  
   December 3, 2009
- NRC Generic Letter 88-17; Loss Of Decay Heat Removal 10 CFR 50.54(f); October 17, 1988  
  - Pro-Line Water Screen Services, Inc.; Installation Of Lower Boot Flapper Seal And Main
- Operations PCRA Backlog Scrub Data; December 23, 2009  
   Frame To Non-Metallic Basket Seals; September 12, 2001
- Point Beach AT-0246 Outage Action Request Mode Change Restraints Data;  
- Rex Chainbelt Inc.; Conveyor And Process Equipment Division Service Manual; June 1965
   December 3, 2009  
- Unified Screw Threads Data; Table 3a - Coarse-Thread Series, UNC And UNRC - Basic
  - Pro-Line Water Screen Services, Inc.; Installation Of Lower Boot Flapper Seal And Main  
   Dimensions; Table 3b - Fine-Thread Series, UNF And UNRF - Basic Dimensions
   Frame To Non-Metallic Basket Seals; September 12, 2001  
1R22 Surveillance Testing
- Rex Chainbelt Inc.; Conveyor And Process Equipment Division Service Manual; June 1965  
- AR 00151138; OSHA Required Crane Inspection Not Performed
- Unified Screw Threads Data; Table 3a - Coarse-Thread Series, UNC And UNRC - Basic  
- AR 01158712; Possible Discrepancies Noted During 2Z-13 Visual Inspection
   Dimensions; Table 3b - Fine-Thread Series, UNF And UNRF - Basic Dimensions
- AR 01158730; 2Z-013 Visually Indeterminable Lateral Support Connections
1R22 Surveillance Testing  
- AR 01158949; 2Z-013 Polar Crane Inspection Weaknesses
- AR 00151138; OSHA Required Crane Inspection Not Performed  
- AR 01159254; 2Z-013 Polar Crane Inspection Weaknesses
- AR 01158712; Possible Discrepancies Noted During 2Z-13 Visual Inspection  
- AR 01159410; Z-013 Main Hoist Has A Pinched Cable
- AR 01158730; 2Z-013 Visually Indeterminable Lateral Support Connections  
- ANSI B30.2.0 - 1976; Overhead And Gantry Cranes (Top Running Bridge, Multiple Girder)
- AR 01158949; 2Z-013 Polar Crane Inspection Weaknesses  
- ASME B30.2-2001; Overhead And Gantry Cranes (Top Running Bridge, Single Or Multiple
- AR 01159254; 2Z-013 Polar Crane Inspection Weaknesses  
   Girder, Top Running Trolley Hoist)
- AR 01159410; Z-013 Main Hoist Has A Pinched Cable  
- ASME B30.2-2005; Overhead And Gantry Cranes (Top Running Bridge, Single Or Multiple
- ANSI B30.2.0 - 1976; Overhead And Gantry Cranes (Top Running Bridge, Multiple Girder)  
   Girder, Top Running Trolley Hoist)
- ASME B30.2-2001; Overhead And Gantry Cranes (Top Running Bridge, Single Or Multiple  
- ASME OM CODE-1995; Code For Operation And Maintenance Of Nuclear Power Plants
   Girder, Top Running Trolley Hoist)  
- AR 01158563; Unit 2 Containment Polar Crane Trolley Failure To Move
- ASME B30.2-2005; Overhead And Gantry Cranes (Top Running Bridge, Single Or Multiple  
- AR 01158730; 2Z-013 - Visually Indeterminable Lateral Support Connection
   Girder, Top Running Trolley Hoist)  
- AR 01158746; Unit 2 Z-13 Crane #1 Controller Bridge Control Broken
- ASME OM CODE-1995; Code For Operation And Maintenance Of Nuclear Power Plants  
- AR 01158788; 2RMP 9118-1 Emergent Issuance
- AR 01158563; Unit 2 Containment Polar Crane Trolley Failure To Move  
- AR 01159790; Polar Crane Stopped Working
- AR 01158730; 2Z-013 - Visually Indeterminable Lateral Support Connection  
- AR 01159794; Potential Improvement To PBV-9240
- AR 01158746; Unit 2 Z-13 Crane #1 Controller Bridge Control Broken  
- AR 01160749; SLP-1 And -2 Conflict With OSHA Required Crane Checks
- AR 01158788; 2RMP 9118-1 Emergent Issuance      
- AR 01160844; Outdated Daily Crane Inspection Form Used
- AR 01159790; Polar Crane Stopped Working  
- AR 01162152; 12L-25 Lighting Panel Breaker Found Tripped
- AR 01159794; Potential Improvement To PBV-9240  
- AR 01162165; AR Not Initiated For Adverse Condition
- AR 01160749; SLP-1 And -2 Conflict With OSHA Required Crane Checks  
- AR 01162167; DC Ground Found During ORT 3A
- AR 01160844; Outdated Daily Crane Inspection Form Used  
- AR 01162172; D-09 AC Input Breaker Tripped
- AR 01162152; 12L-25 Lighting Panel Breaker Found Tripped  
- AR 01162173; Sliders Found Open During RF-445
- AR 01162165; AR Not Initiated For Adverse Condition  
- AR 01162177; G-01 Alarms Received During ORT 3A
- AR 01162167; DC Ground Found During ORT 3A  
- AR 01162205; Use Of CAPs Not Reinforced In ORT 3A
- AR 01162172; D-09 AC Input Breaker Tripped  
- AR 01162206; SA-51 Interstage Bleed On K-3B SA Compressor Does Not Work
- AR 01162173; Sliders Found Open During RF-445  
                                              11                                  Attachment
- AR 01162177; G-01 Alarms Received During ORT 3A  
- AR 01162205; Use Of CAPs Not Reinforced In ORT 3A  
- AR 01162206; SA-51 Interstage Bleed On K-3B SA Compressor Does Not Work  


- AR 01162212; Unexpected Alarm, 2C20A 2-2, D-01/D-03 DC Bus Under Voltage
- AR 01162222; Full Shut 2MS-5958 Indicates 12% Open Locally During ORT-54
12
- AR 01162638; 2DT-2081 Gasket Failure
Attachment
- AR 01162668; 2P029T Oil Sample Contained Water
- AR 01162212; Unexpected Alarm, 2C20A 2-2, D-01/D-03 DC Bus Under Voltage  
- AR 01162712; 2MS-2082 Trip Valve Leakage Observed During IT 09A
- AR 01162222; Full Shut 2MS-5958 Indicates 12% Open Locally During ORT-54  
- AR 01162728; TS-81 G-01 EDG Testing While 2P-29 TDAFW Pump OOS
- AR 01162638; 2DT-2081 Gasket Failure  
- AR 01162762; OBD Completion Did Not Reverse Changes To Procedure
- AR 01162668; 2P029T Oil Sample Contained Water  
- CMP 11.1; Component Maintenance Program; Revision 0
- AR 01162712; 2MS-2082 Trip Valve Leakage Observed During IT 09A  
- FSAR Appendix A.3; Control Of Heavy Loads
- AR 01162728; TS-81 G-01 EDG Testing While 2P-29 TDAFW Pump OOS  
- IT 09A; Cold Start Of Turbine-Driven Auxiliary Feed Pump And Valve Test (Quarterly) Unit 2;
- AR 01162762; OBD Completion Did Not Reverse Changes To Procedure  
   Revision 49
- CMP 11.1; Component Maintenance Program; Revision 0  
- ORT 3A; Safety Injection Actuation With Loss Of Engineered Safeguards AC (Train A)
- FSAR Appendix A.3; Control Of Heavy Loads  
- NRC Correspondence To Wisconsin Electric Power Company; February 1, 1982
- IT 09A; Cold Start Of Turbine-Driven Auxiliary Feed Pump And Valve Test (Quarterly) Unit 2;  
- NUREG-0612; Control Of Heavy Loads At Nuclear Power Plants
   Revision 49  
- 2RMP 9118-1; Containment Building Crane OSHA Operability Inspections; Revision 5
- ORT 3A; Safety Injection Actuation With Loss Of Engineered Safeguards AC (Train A)
- SLP 10; Load Weight Listings And Rigging Figures; Revision 22
- NRC Correspondence To Wisconsin Electric Power Company; February 1, 1982  
- WO 359117; Wire Rope Inspection
- NUREG-0612; Control Of Heavy Loads At Nuclear Power Plants  
- ALPS Wire Rope Corporation; Certificate Of Conformance; October 25, 2009
- 2RMP 9118-1; Containment Building Crane OSHA Operability Inspections; Revision 5  
- Control Room Log Entries Data; TDAFW Test; December 4 - 11, 2009
- SLP 10; Load Weight Listings And Rigging Figures; Revision 22  
- Drawing 275460; Auxiliary Feedwater System Units 1 and 2
- WO 359117; Wire Rope Inspection  
- Point Beach Nuclear Plant Wire Rope Inspection Criteria Instructions
- ALPS Wire Rope Corporation; Certificate Of Conformance; October 25, 2009  
- Priority Work Schedule Data; September 10, 2009
- Control Room Log Entries Data; TDAFW Test; December 4 - 11, 2009  
1EP2 Alert and Notification Evaluation
- Drawing 275460; Auxiliary Feedwater System Units 1 and 2  
- ENS Notification 45553; Notification Due To A Single Emergency Siren Actuation;
- Point Beach Nuclear Plant Wire Rope Inspection Criteria Instructions  
   December 9, 2009
- Priority Work Schedule Data; September 10, 2009  
- EPMP 6.0; Alert And Notification System; Revision 9
1EP2 Alert and Notification Evaluation  
- FEMA Prompt Alert And Notification System Approval Letter And Design Report;
- ENS Notification 45553; Notification Due To A Single Emergency Siren Actuation;  
   December 7, 1987
   December 9, 2009  
- PBNP ANS Maintenance Records; October 2007 - November 2009
- EPMP 6.0; Alert And Notification System; Revision 9  
- AR 01162916; Power Outages Caused Sever Sirens Out-of-Service Due To Weather
- FEMA Prompt Alert And Notification System Approval Letter And Design Report;  
- AR 01160553; Replaced Siren P-013 Antenna
   December 7, 1987  
- AR 01130759; Siren Test Postponed Due To Severe Weather
- PBNP ANS Maintenance Records; October 2007 - November 2009  
1EP3 Emergency Response Organization Augmentation Testing
- AR 01162916; Power Outages Caused Sever Sirens Out-of-Service Due To Weather  
- EP 5.0; Organizational Control Of Emergencies; Revision 52
- AR 01160553; Replaced Siren P-013 Antenna  
- EPIP 1.1; ERO Notification; Revision 56
- AR 01130759; Siren Test Postponed Due To Severe Weather  
- EPG 1.0; Point Beach Nuclear Plant Shift Augmentation Drill Guideline; Revision 13
1EP3 Emergency Response Organization Augmentation Testing  
- EPMP 7.0; Emergency Response Organization Notification System; Revision 6
- EP 5.0; Organizational Control Of Emergencies; Revision 52  
- PBN EP TP; Emergency Preparedness Training Program Description; Revision 8
- EPIP 1.1; ERO Notification; Revision 56  
- Emergency Response Organization Training Drill Team Roster; December 3, 2009
- EPG 1.0; Point Beach Nuclear Plant Shift Augmentation Drill Guideline; Revision 13  
- LMS ERO Qualification Status Verification; December 10, 2009
- EPMP 7.0; Emergency Response Organization Notification System; Revision 6  
- NPM 2008-0130; March 27, Quarterly ERO Augmentation Drills;
- PBN EP TP; Emergency Preparedness Training Program Description; Revision 8  
   May 2, 2008 - September 17, 2009
- Emergency Response Organization Training Drill Team Roster; December 3, 2009  
- AR 01162982; Augmentation Drills Taking Credit For 30-Minute Chemistry Technician With
- LMS ERO Qualification Status Verification; December 10, 2009  
  On-shift Chemistry Technician
- NPM 2008-0130; March 27, Quarterly ERO Augmentation Drills;  
- AR 01162977; Augmentation Drill Start Time Questioned During NRC Inspection
   May 2, 2008 - September 17, 2009  
- AR 01162972; Loss Of Dialogics ERO Notification System Capabilities
- AR 01162982; Augmentation Drills Taking Credit For 30-Minute Chemistry Technician With  
- AR 01155763; EP ERO Expectations For Wearing A Pager
On-shift Chemistry Technician  
                                              12                                  Attachment
- AR 01162977; Augmentation Drill Start Time Questioned During NRC Inspection  
- AR 01162972; Loss Of Dialogics ERO Notification System Capabilities  
- AR 01155763; EP ERO Expectations For Wearing A Pager  


- AR 01153790; July 28, 2009 Drill Dose Assessment Challenge
- AR 01156706; September 17, 2009 Augmentation Drill Two Responders Greater Than
13
  30 Minutes And One Responder Greater Than 60 Minutes
Attachment
- AR 01151489; June 16, 2009 ERO Augmentation Drill Two Responders Greater Than
- AR 01153790; July 28, 2009 Drill Dose Assessment Challenge  
  30 Minutes
- AR 01156706; September 17, 2009 Augmentation Drill Two Responders Greater Than  
1EP4 Emergency Action Level And Emergency Plan Changes
30 Minutes And One Responder Greater Than 60 Minutes  
- EP 2.0; Emergency Plan Acronyms And Definitions; 41 and 42
- AR 01151489; June 16, 2009 ERO Augmentation Drill Two Responders Greater Than  
- EP 6.0; Emergency Measures; 50, 51, and 52
30 Minutes  
- EPIP 1.2.1; Emergency Action Level Technical Basis; 3
1EP4 Emergency Action Level And Emergency Plan Changes  
- 10 CFR 50.54(q) Reviews For Emergency Plan And EAL Revisions
- EP 2.0; Emergency Plan Acronyms And Definitions; 41 and 42  
1EP5 Correction Of Emergency Preparedness Weaknesses And Deficiencies
- EP 6.0; Emergency Measures; 50, 51, and 52  
- Focused Self-Assessment Report PBSA-EP-09-03; Point Beach Emergency Preparedness
- EPIP 1.2.1; Emergency Action Level Technical Basis; 3  
  Pre-NRC Inspection; November 3, 2009
- 10 CFR 50.54(q) Reviews For Emergency Plan And EAL Revisions  
- Point Beach Toxic Gas Unusual Event July 3, 2008 Report; July 14, 2008
1EP5 Correction Of Emergency Preparedness Weaknesses And Deficiencies  
- Point Beach Security Unusual Event April 8, 2008 Report; May 7, 2008
- Focused Self-Assessment Report PBSA-EP-09-03; Point Beach Emergency Preparedness  
- Point Beach Loss Of Off-Site Power Unusual Event January 15, 2008 Report;
Pre-NRC Inspection; November 3, 2009  
  February 26, 2008
- Point Beach Toxic Gas Unusual Event July 3, 2008 Report; July 14, 2008  
- PBNP 09-026; Emergency Preparedness Audit; August 12, 2009
- Point Beach Security Unusual Event April 8, 2008 Report; May 7, 2008  
- PBNP 08-026; Emergency Preparedness Assessment; August 12, 2008
- Point Beach Loss Of Off-Site Power Unusual Event January 15, 2008 Report;  
- PBNP 08-011; Emergency Preparedness Assessment; May 3, 2008
February 26, 2008  
- AR 01151074; EPlan Organization Chart Different Than Site Organization Chart
- PBNP 09-026; Emergency Preparedness Audit; August 12, 2009  
- AR 01149526; Radiation Protection Leader Position Drops Below Three Deep
- PBNP 08-026; Emergency Preparedness Assessment; August 12, 2008  
- AR 01136999; Self-Assessment DEP Data Discrepancy
- PBNP 08-011; Emergency Preparedness Assessment; May 3, 2008  
- AR 01131429; July 3, 2008 Evaluate Toxic Gas EAL
- AR 01151074; EPlan Organization Chart Different Than Site Organization Chart  
- AR 01131394; July 3, 2008 Unusual Event
- AR 01149526; Radiation Protection Leader Position Drops Below Three Deep  
- AR 01121253; Transfer Of Command And Control Confusion During January 15, 2008
- AR 01136999; Self-Assessment DEP Data Discrepancy  
  Unusual Event
- AR 01131429; July 3, 2008 Evaluate Toxic Gas EAL  
- AR 01120314; Unusual Event January 15, 2008 ENS Notification Made At 59 Minutes
- AR 01131394; July 3, 2008 Unusual Event  
2OS1 Access Control to Radiologically Significant Areas
- AR 01121253; Transfer Of Command And Control Confusion During January 15, 2008  
- RWP 00000861, Fuel Motion And Sent Fuel Pool Activities; Revision 1
Unusual Event  
- HP 2.14; Containment Keyway Personnel Access; Revision 15
- AR 01120314; Unusual Event January 15, 2008 ENS Notification Made At 59 Minutes  
- HP 2.15.1; High Level Contamination And Discrete Radioactive Particle Control; Revision 5
2OS1 Access Control to Radiologically Significant Areas  
- HP 2.17; Very High Radiation Area Personnel Access; Revision 7
- RWP 00000861, Fuel Motion And Sent Fuel Pool Activities; Revision 1  
- HP 2.6; Locked And Very High Radiation Area Key Control; Revision 32
- HP 2.14; Containment Keyway Personnel Access; Revision 15  
- HP 3.2; Radiological Labeling, Posting And Barricading Requirements; Revision 50
- HP 2.15.1; High Level Contamination And Discrete Radioactive Particle Control; Revision 5  
- HP 3.2.10; Secure High Radiation Area Controls; Revision 1
- HP 2.17; Very High Radiation Area Personnel Access; Revision 7  
- HP 3.6; Alpha Monitoring Program; Revision 0
- HP 2.6; Locked And Very High Radiation Area Key Control; Revision 32  
- HPIP 1.64; Control of Underwater Diving In Radiologically Hazardous Areas; Revision 7
- HP 3.2; Radiological Labeling, Posting And Barricading Requirements; Revision 50  
- HPIP 2.1.1; Response Checks Of Portable Survey Instruments; Revision 11
- HP 3.2.10; Secure High Radiation Area Controls; Revision 1  
- HPIP 3.50; Radiation Surveys; Revision 13
- HP 3.6; Alpha Monitoring Program; Revision 0  
- FP-RP-JPP-01; Radiation Protection Job Planning; Revision 6
- HPIP 1.64; Control of Underwater Diving In Radiologically Hazardous Areas; Revision 7  
- 0-SOP-FH-001; Fuel/Insert/Component Movement In the Spent Fuel Pool Or New Fuel Vault;
- HPIP 2.1.1; Response Checks Of Portable Survey Instruments; Revision 11  
  Revision 15
- HPIP 3.50; Radiation Surveys; Revision 13  
- RP 1C, Refueling; Revision 65
- FP-RP-JPP-01; Radiation Protection Job Planning; Revision 6  
- RP 2A; Receipt Of New Fuel Assemblies; Revision 47
- 0-SOP-FH-001; Fuel/Insert/Component Movement In the Spent Fuel Pool Or New Fuel Vault;  
                                              13                                  Attachment
Revision 15  
- RP 1C, Refueling; Revision 65  
- RP 2A; Receipt Of New Fuel Assemblies; Revision 47  


- RP-18 Part 3; Place Loaded DSC/TC Back Into The Spent Fuel Pool; Revision 3
- RESP- 2.3; Defective Removable Top Nozzle Replacement; Revision 7
14
- HPCAL 1.1; Radiation Protection Instrument Calibration, Repair And Response Checks;
Attachment
  Revision 22
- RP-18 Part 3; Place Loaded DSC/TC Back Into The Spent Fuel Pool; Revision 3  
- NP 4.2.19; Entry Requirements Into Various Radiologically Controlled Areas; Revision 16
- RESP- 2.3; Defective Removable Top Nozzle Replacement; Revision 7  
- NP 4.2.32; Respiratory Protection Program; Revision 7
- HPCAL 1.1; Radiation Protection Instrument Calibration, Repair And Response Checks;  
- AR SAR 01142742; Access Control To Radiologically Significant Areas And ALARA Planning
Revision 22  
  And Controls
- NP 4.2.19; Entry Requirements Into Various Radiologically Controlled Areas; Revision 16  
- AR SAR 0115197; Access Control To Radiologically Significant Areas And ALARA Planning
- NP 4.2.32; Respiratory Protection Program; Revision 7  
  And Controls
- AR SAR 01142742; Access Control To Radiologically Significant Areas And ALARA Planning  
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls
And Controls  
- FP-WM-PLA-01; Work Order Planning Process; 5
- AR SAR 0115197; Access Control To Radiologically Significant Areas And ALARA Planning  
- NP 4.2.1; ALARA Program; Revision 20
And Controls  
- FP-RP-JPP-01; RP Job Planning; Revision 6
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls  
- FP-RP-RWP-01; Radiation Work Permit; Revision 8
- FP-WM-PLA-01; Work Order Planning Process; 5  
- Radiological Controls And Associated ALARA Files For Insulation; Work Orders 00371055,
- NP 4.2.1; ALARA Program; Revision 20  
  00371056, And 00371057
- FP-RP-JPP-01; RP Job Planning; Revision 6  
- Radiological Controls And Associated ALARA Files For RCP Work; Work Orders 00356469,
- FP-RP-RWP-01; Radiation Work Permit; Revision 8  
  00358775, And 00366298
- Radiological Controls And Associated ALARA Files For Insulation; Work Orders 00371055,  
- Radiological Controls And Associated ALARA Files For Core Barrel Move; Work Order
00371056, And 00371057  
  00365421
- Radiological Controls And Associated ALARA Files For RCP Work; Work Orders 00356469,  
4OA1 Performance Indicator Verification
00358775, And 00366298  
- 2-PT-AF-2; Turbine Driven Auxiliary Feedwater System And MS Supply Pressure Test Outside
- Radiological Controls And Associated ALARA Files For Core Barrel Move; Work Order  
   Containment - Unit 2
00365421  
- AR 01135651; AF Mod Deferral Requires MSPI Basis Document Update
4OA1 Performance Indicator Verification  
- AR 01138122; PRA Change For MSPI Not Explained In Submittal File
- 2-PT-AF-2; Turbine Driven Auxiliary Feedwater System And MS Supply Pressure Test Outside  
- AR 01138400; PRA Change For MSPI Not Explained In Submittal File
   Containment - Unit 2  
- AR 01142718; MSPI Margin Reduced Due To PRA Change
- AR 01135651; AF Mod Deferral Requires MSPI Basis Document Update  
- EPG 1.1; Performance Indicator Guideline; Revision 6
- AR 01138122; PRA Change For MSPI Not Explained In Submittal File  
- EPMP 6.0; Alert And Notification System Siren Function Data; October 2008 -
- AR 01138400; PRA Change For MSPI Not Explained In Submittal File  
  September 2009
- AR 01142718; MSPI Margin Reduced Due To PRA Change  
- FG-E-MSPI-01; Mitigating System Performance Index; Revision 3
- EPG 1.1; Performance Indicator Guideline; Revision 6  
- LI-AA-200-1000-10000; FPL Fleet Licensing Performance Indicators; Revision 00
- EPMP 6.0; Alert And Notification System Siren Function Data; October 2008 -  
- Mitigating Systems Performance Index (MSPI) Basis Document Data For Point Beach Nuclear
September 2009  
   Plant; Revisions 12 And 14
- FG-E-MSPI-01; Mitigating System Performance Index; Revision 3  
- MSPI Monthly Unavailability And Verification Data; July, August, And September, 2008
- LI-AA-200-1000-10000; FPL Fleet Licensing Performance Indicators; Revision 00  
- MSPI Monthly Unavailability And Verification Data; October, November, And December, 2008
- Mitigating Systems Performance Index (MSPI) Basis Document Data For Point Beach Nuclear  
- MSPI Monthly Unavailability And Verification Data; January, February, And March, 2009
   Plant; Revisions 12 And 14  
- MSPI Monthly Unavailability And Verification Data; April, May, And June, 2009
- MSPI Monthly Unavailability And Verification Data; July, August, And September, 2008  
- NP 5.2.16; NRC Performance Indicators; Revision 14
- MSPI Monthly Unavailability And Verification Data; October, November, And December, 2008  
- NRC Occupational Exposure Performance Indicator Data; October 2008 Through
- MSPI Monthly Unavailability And Verification Data; January, February, And March, 2009  
   September 2009
- MSPI Monthly Unavailability And Verification Data; April, May, And June, 2009  
- Alert and Notification System Performance Indicator Records; October 2008 -
- NP 5.2.16; NRC Performance Indicators; Revision 14  
  September 2009
- NRC Occupational Exposure Performance Indicator Data; October 2008 Through  
- Atmospheric Effluent Radioisotopic Quantification Report; March 2009
   September 2009  
- Atmospheric Effluent Radioisotopic Quantification Report; June 2009
- Alert and Notification System Performance Indicator Records; October 2008 -  
- Atmospheric Effluent Radioisotopic Quantification Report; September 2009
September 2009  
                                              14                                    Attachment
- Atmospheric Effluent Radioisotopic Quantification Report; March 2009  
- Atmospheric Effluent Radioisotopic Quantification Report; June 2009  
- Atmospheric Effluent Radioisotopic Quantification Report; September 2009  


- Drill And Exercise Performance PI Results; October 2008 - September 2009
- Drill And Exercise Performance Records; October 2008 - September 2009
15
- ERO Drill Participation Summaries; December 2008 - September 2009
Attachment
- ERO Participation Monthly Reports; December 2008 - September 2009
- Drill And Exercise Performance PI Results; October 2008 - September 2009  
- Emergency Preparedness Attendance Reports; December 2008 - September 2009
- Drill And Exercise Performance Records; October 2008 - September 2009  
- Liquid Effluent Radioisotopic Quantification Report; March 2009
- ERO Drill Participation Summaries; December 2008 - September 2009  
- Liquid Effluent Radioisotopic Quantification Report; June 2009
- ERO Participation Monthly Reports; December 2008 - September 2009  
- Liquid Effluent Radioisotopic Quantification Report; September 2009
- Emergency Preparedness Attendance Reports; December 2008 - September 2009  
- Mitigating Systems Performance Index Derivation Report Units 1 And 2; Heat Removal
- Liquid Effluent Radioisotopic Quantification Report; March 2009  
   System; Third Quarter of 2008 Through Second Quarter of 2009
- Liquid Effluent Radioisotopic Quantification Report; June 2009  
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 5
- Liquid Effluent Radioisotopic Quantification Report; September 2009  
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 6;
- Mitigating Systems Performance Index Derivation Report Units 1 And 2; Heat Removal  
   October 2009
   System; Third Quarter of 2008 Through Second Quarter of 2009
- NP 1.10.1; Record Keeping For NRC Licensed Operators; Revision 8
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 5  
- NP 5.2.16; NRC Performance Indicators; Revision 14
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 6;
- NP 5.2.17; Equipment Performance And Information Exchange (EPIX); Revision 2
   October 2009  
- OI 62A; Motor-Driven Auxiliary Feedwater System (P-38A And P-38B)
- NP 1.10.1; Record Keeping For NRC Licensed Operators; Revision 8  
- TRHB 11.4; Secondary Systems Descriptions: Auxiliary Feedwater System; Revision 10
- NP 5.2.16; NRC Performance Indicators; Revision 14  
- Control Room Log Entries; July 2008 through June 2009
- NP 5.2.17; Equipment Performance And Information Exchange (EPIX); Revision 2  
4OA2 Identification and Resolution of Problems
- OI 62A; Motor-Driven Auxiliary Feedwater System (P-38A And P-38B)  
- AR 01114734; Lack Of Progress On Cable Submergence Issue
- TRHB 11.4; Secondary Systems Descriptions: Auxiliary Feedwater System; Revision 10  
- AR 01163603; Trend Coding Of CAPS
- Control Room Log Entries; July 2008 through June 2009
- AR 01138519; FM Found During Lower Core Plate Inspection
4OA2 Identification and Resolution of Problems  
- AR 01157789; FME Barrier Found Inside FW Heater 4A During Inspection
- AR 01114734; Lack Of Progress On Cable Submergence Issue  
- AR 01158516; Component Cooling Water Heat Exchanger FME Issues
- AR 01163603; Trend Coding Of CAPS  
- AR 01158573; Wrench Dropped Into Cavity
- AR 01138519; FM Found During Lower Core Plate Inspection  
- AR 01159958; Foreign Material Found In Discharge Of 2CV-257
- AR 01157789; FME Barrier Found Inside FW Heater 4A During Inspection  
- AR 01160348; FM Debris Scan Challenged RV Lower Internal Install (2R30)
- AR 01158516; Component Cooling Water Heat Exchanger FME Issues  
- AR 01160355; LUVS Screen Dropped In Refuel Cavity
- AR 01158573; Wrench Dropped Into Cavity  
- AR 01160443; Found Washer Between Gasket And Flange Face On 2HX-15A3
- AR 01159958; Foreign Material Found In Discharge Of 2CV-257  
- AR 01160489; Foreign Material On Lower Core Plate
- AR 01160348; FM Debris Scan Challenged RV Lower Internal Install (2R30)  
- AR 01160494; Trend - Submerged Electrical Cables
- AR 01160355; LUVS Screen Dropped In Refuel Cavity  
- AR 01160572; Resource Needs Were Not Identified To Support FM Inspection In RMP
- AR 01160443; Found Washer Between Gasket And Flange Face On 2HX-15A3  
- AR 01160820; U2R30 Cavity Foreign Material Controls
- AR 01160489; Foreign Material On Lower Core Plate  
- AR 01160980; SFMEA Concerns At The Spent Fuel Pool
- AR 01160494; Trend - Submerged Electrical Cables  
- AR 01161181; Untimely Reporting Of foreign Material
- AR 01160572; Resource Needs Were Not Identified To Support FM Inspection In RMP  
- AR 01161214; Z-756 Hoist Pendant Damage Causes Hoist Inoperability
- AR 01160820; U2R30 Cavity Foreign Material Controls  
- AR 01161216; FME Found While Inspecting Portion Of 2A02 Bus
- AR 01160980; SFMEA Concerns At The Spent Fuel Pool  
- AR 01161285; Sump Bravo Needs Fabricated FME Covers When Elbows Are Removed
- AR 01161181; Untimely Reporting Of foreign Material  
- AR 01161310; During 2ICP 02.019 Testing, We Found A Hair In PC-949B-XA
- AR 01161214; Z-756 Hoist Pendant Damage Causes Hoist Inoperability  
- AR 01161672; Bechtel Contamination Control For Valves And Pipes
- AR 01161216; FME Found While Inspecting Portion Of 2A02 Bus  
- AR 01162133; Foreign Material Found In The New Output Breakers
- AR 01161285; Sump Bravo Needs Fabricated FME Covers When Elbows Are Removed  
- AR 01162169; FME Issue Of Bottle Dropped In Stabrex Tanker
- AR 01161310; During 2ICP 02.019 Testing, We Found A Hair In PC-949B-XA  
- AR 01162213; No Housing Covers Installed On FD Valve Operators
- AR 01161672; Bechtel Contamination Control For Valves And Pipes  
- AR 01162509; Four Absorbent Bags Found In the Unit 2 Turbine Hall Sump
- AR 01162133; Foreign Material Found In The New Output Breakers  
- CMP 12.0; Equipment Failure Trending; Revision 5
- AR 01162169; FME Issue Of Bottle Dropped In Stabrex Tanker  
- FG-PA-CTC-01; CAP Trend Code Manual; Revision 11
- AR 01162213; No Housing Covers Installed On FD Valve Operators  
- FG-PA-DRUM-01; Department Roll Up Meeting Manual - Department Performance Trending;
- AR 01162509; Four Absorbent Bags Found In the Unit 2 Turbine Hall Sump  
  Revision 8
- CMP 12.0; Equipment Failure Trending; Revision 5  
                                                15                              Attachment
- FG-PA-CTC-01; CAP Trend Code Manual; Revision 11  
- FG-PA-DRUM-01; Department Roll Up Meeting Manual - Department Performance Trending;  
Revision 8  


- PBN-09-010; Point Beach Nuclear Assurance Report; System Engineering; May 26, 2009
- REI 48.0; Reactor Engineering Trending Program; Revision 2
16
- Point Beach Nuclear Plant AT-0384 Activity Trending Data; December 21, 2009
Attachment
- Point Beach Nuclear Plant Drum Summary Report; First Quarter 2009
- PBN-09-010; Point Beach Nuclear Assurance Report; System Engineering; May 26, 2009  
- Point Beach Nuclear Plant Drum Summary Report; Second Quarter 2009
- REI 48.0; Reactor Engineering Trending Program; Revision 2  
4OA5 Other Activities
- Point Beach Nuclear Plant AT-0384 Activity Trending Data; December 21, 2009  
- AR 01165164; NP-413 Policy Requirement Not Implemented
- Point Beach Nuclear Plant Drum Summary Report; First Quarter 2009  
- Policy HR-AA-01; Involuntary Termination Or Other Significant Employment Actions Affecting
- Point Beach Nuclear Plant Drum Summary Report; Second Quarter 2009  
  Nuclear Division Employees; Revision 0
4OA5 Other Activities  
- Policy SY-AA-02; Denial of Unescorted Access to FPL/FPLE Nuclear Facility; Revision 0
- AR 01165164; NP-413 Policy Requirement Not Implemented  
- FP&L NUC GET Plant Access Training 003; Revision Dated July 26, 2006
- Policy HR-AA-01; Involuntary Termination Or Other Significant Employment Actions Affecting  
- HPIP 1.60; Calculating Shallow And Deep Dose Rates Due To Skin Contamination;
Nuclear Division Employees; Revision 0  
   Revision 11
- Policy SY-AA-02; Denial of Unescorted Access to FPL/FPLE Nuclear Facility; Revision 0  
- NP 1.7.3; Site Specific Requirements For Access To And Termination From Point Beach
- FP&L NUC GET Plant Access Training 003; Revision Dated July 26, 2006  
  Nuclear Plant; Revision 18
- HPIP 1.60; Calculating Shallow And Deep Dose Rates Due To Skin Contamination;  
- NP 4.2.25; Release Of Material, Equipment And Personal Items From The Radiologically
   Revision 11  
  Controlled Areas; Revision 14
- NP 1.7.3; Site Specific Requirements For Access To And Termination From Point Beach  
- Apparent Cause Evaluation - AR 01150045; Loss Of Radioactive Material Control Inside
Nuclear Plant; Revision 18
  Protected Area; Revision 1 and 2
- NP 4.2.25; Release Of Material, Equipment And Personal Items From The Radiologically  
- Chesapeake Nuclear Services Final Report, Dose Assessment For May 21, 2009
Controlled Areas; Revision 14  
  Contamination Event At The Point Beach Nuclear Plant; September 10, 2009
- Apparent Cause Evaluation - AR 01150045; Loss Of Radioactive Material Control Inside  
- Dispersed Contamination Dose Assessment Summary; July 2, 2009
Protected Area; Revision 1 and 2  
- Personnel Contamination Event Report; May 21, 2009
- Chesapeake Nuclear Services Final Report, Dose Assessment For May 21, 2009  
- DRW 110E029, Sheet 1; Auxiliary Coolant System; September 10, 2008.
Contamination Event At The Point Beach Nuclear Plant; September 10, 2009  
- DRW 110E035, Sheet 1; Safety Injection System; August 1, 2007
- Dispersed Contamination Dose Assessment Summary; July 2, 2009  
- DRW P-248; Residual Heat Removal System; December 25, 1999
- Personnel Contamination Event Report; May 21, 2009  
- DRW P-237; SIS to Primary Coolant Cold Leg; January 22, 2004
- DRW 110E029, Sheet 1; Auxiliary Coolant System; September 10, 2008.  
- PO No. 00024065; Point Beach Walkdown Closure Report; November 16, 2009
- DRW 110E035, Sheet 1; Safety Injection System; August 1, 2007  
- AR 01129366; PBNP Confirmatory Order Requirements Sustainability For Adverse
- DRW P-248; Residual Heat Removal System; December 25, 1999  
  Employment Actions
- DRW P-237; SIS to Primary Coolant Cold Leg; January 22, 2004  
- AR 01129462; Schedule For Incumbent Mgrs/Supv For NLA Course
- PO No. 00024065; Point Beach Walkdown Closure Report; November 16, 2009  
- AR 01129565; 4 Individuals Not Meeting SCWE Confirmatory Order
- AR 01129366; PBNP Confirmatory Order Requirements Sustainability For Adverse  
- AR 01129659; EA 06-178 Confirmatory Order Inspection Finding
Employment Actions  
- AR 01152228; Independent Assessment Of The Effectiveness Of Corrective Actions From
- AR 01129462; Schedule For Incumbent Mgrs/Supv For NLA Course  
  Safety Culture Survey
- AR 01129565; 4 Individuals Not Meeting SCWE Confirmatory Order  
- AR 01157190; Schedule PBN Personnel For SDA/LF Slots
- AR 01129659; EA 06-178 Confirmatory Order Inspection Finding  
- AR 01157534; Quick Hit Assessment PBSA-SRC-09-04
- AR 01152228; Independent Assessment Of The Effectiveness Of Corrective Actions From  
- AR 01162560; Security Supervisor Not Tracked For Required SCWE Training
Safety Culture Survey  
- AR 01162564; 7 People Required To Attend SCWE Training And Not Being Tracked
- AR 01157190; Schedule PBN Personnel For SDA/LF Slots  
- AR 01163410; Follow-up Issue SCWE Confirmatory Order Inspection
- AR 01157534; Quick Hit Assessment PBSA-SRC-09-04  
- FPL Nuclear Policy NP-413; Involuntary Termination of Division Employees; Revision 5
- AR 01162560; Security Supervisor Not Tracked For Required SCWE Training  
- NMC Policy CP 0087; Material Employment Action Review; Revision 0
- AR 01162564; 7 People Required To Attend SCWE Training And Not Being Tracked  
- Corrective Action Effectiveness Review -AR01070153-12, April 29, 2009
- AR 01163410; Follow-up Issue SCWE Confirmatory Order Inspection  
- Memo from F. Flentje to J. Costedio; Verification of 2007 SCWE Confirmatory Order Actions
- FPL Nuclear Policy NP-413; Involuntary Termination of Division Employees; Revision 5  
  Committed During September, 24, 2008 Public Meeting with NRC; February 14, 2009
- NMC Policy CP 0087; Material Employment Action Review; Revision 0  
- PARB Presentation for Non-Performance of EFR 1070334, Adverse Employment Action
- Corrective Action Effectiveness Review -AR01070153-12, April 29, 2009
  Policy, November 30, 2007
- Memo from F. Flentje to J. Costedio; Verification of 2007 SCWE Confirmatory Order Actions  
- Memo from B. Deuel to Nuclear Safety Culture Improvement Team; September 30, 2009
Committed During September, 24, 2008 Public Meeting with NRC; February 14, 2009  
  Nuclear Safety Culture Improvement Team Meeting Minutes; September 30, 2009
- PARB Presentation for Non-Performance of EFR 1070334, Adverse Employment Action  
                                              16                                Attachment
Policy, November 30, 2007  
- Memo from B. Deuel to Nuclear Safety Culture Improvement Team; September 30, 2009  
Nuclear Safety Culture Improvement Team Meeting Minutes; September 30, 2009  


- Memo from B. Deuel to Nuclear Safety Culture Improvement Team; December 2, 2009
  Nuclear Safety Culture Improvement Team Meeting Minutes; December 2, 2009
17
- Memo from L Meyer to File; August 2009 PBNP PTAB Meeting Minutes; September 12, 2009
Attachment
- Memo from L Meyer to File; February 2009 PBNP PTAB Meeting Minutes; February 23, 2009
- Memo from B. Deuel to Nuclear Safety Culture Improvement Team; December 2, 2009  
- Point Beach Supervisor Leadership Development Program; Training Program Description;
Nuclear Safety Culture Improvement Team Meeting Minutes; December 2, 2009  
  Revision 6
- Memo from L Meyer to File; August 2009 PBNP PTAB Meeting Minutes; September 12, 2009  
- Point Beach Succession Plan; January 2010
- Memo from L Meyer to File; February 2009 PBNP PTAB Meeting Minutes; February 23, 2009  
- Point Beach Knowledge Retention Program; December 2009
- Point Beach Supervisor Leadership Development Program; Training Program Description;  
- NRC 2007-0015, NMC Letter to NRC; NMC Plan to Address the Safety Culture Issues an at
Revision 6  
  Point Beach Nuclear Plant; March 29, 2007 (ML070890434)
- Point Beach Succession Plan; January 2010  
- NRC 2008-0078, FPL Energy Letter to NRC; Status of Action Plans Taken in Response to
- Point Beach Knowledge Retention Program; December 2009  
  Confirmatory Order EA-06-178; November 11, 2008 (ML083170356)
- NRC 2007-0015, NMC Letter to NRC; NMC Plan to Address the Safety Culture Issues an at  
- NRC 2008-0090, FPL Energy Letter to NRC; Confirmatory Order EA-06-178 Section IV.6
Point Beach Nuclear Plant; March 29, 2007 (ML070890434)  
  Nuclear Safety Culture Survey Results; December 22, 2008 (ML083660387)
- NRC 2008-0078, FPL Energy Letter to NRC; Status of Action Plans Taken in Response to  
- Point Beach Independent Assessment of Safety Culture Survey Corrective Action
Confirmatory Order EA-06-178; November 11, 2008 (ML083170356)  
  Effectiveness; June 28, 2009
- NRC 2008-0090, FPL Energy Letter to NRC; Confirmatory Order EA-06-178 Section IV.6  
                                            17                                Attachment
Nuclear Safety Culture Survey Results; December 22, 2008 (ML083660387)  
- Point Beach Independent Assessment of Safety Culture Survey Corrective Action  
Effectiveness; June 28, 2009  


                          LIST OF ACRONYMS USED
AC   Alternating Current
18
ACE   Apparent Cause Evaluation
Attachment
ADAMS Agencywide Document Access Management System
LIST OF ACRONYMS USED
ADR   Alternative Dispute Resolution
AC  
AFW   Auxiliary Feedwater
Alternating Current  
ALARA As-Low-As-Is-Reasonably-Achievable
ACE  
ANS   Alert and Notification System
Apparent Cause Evaluation  
AOV   Air Operated Valve
ADAMS  
AR   Action Request
Agencywide Document Access Management System  
ASME American Society of Mechanical Engineers
ADR  
AV   Apparent Violation
Alternative Dispute Resolution  
BACC Boric Acid Corrosion Control
AFW  
CAP   Corrective Action Program
Auxiliary Feedwater  
CCWHX Component Cooling Water Hear Exchanger
ALARA  
CFC   Containment Fan Cooler
As-Low-As-Is-Reasonably-Achievable  
CFR   Code of Federal Regulations
ANS  
EA   Enforcement Action
Alert and Notification System  
EC   Engineering Change
AOV  
EDE   Effective Dose Equivalent
Air Operated Valve  
ELHX Excess Letdown Heat Exchanger
AR  
EP   Emergency Preparedness
Action Request  
EPRI Electric Power Research Institute
ASME  
EPU   Extended Power Up-Rate
American Society of Mechanical Engineers  
ERO   Emergency Response Organization
AV  
FPL   Florida Power and Light
Apparent Violation  
FSAR Final Safety Analysis Report
BACC  
FW   Feedwater
Boric Acid Corrosion Control  
GL   Generic Letter
CAP  
GSI   Generic Safety Issue
Corrective Action Program  
I&C   Instrumentation and Control
CCWHX  
IEL   Initiating Event Likelihood
Component Cooling Water Hear Exchanger  
IMC   Inspection Manual Chapter
CFC  
IP   Inspection Procedure
Containment Fan Cooler  
IR   Inspection Report
CFR  
ISI   Inservice Inspection
Code of Federal Regulations  
LER   Licensee Event Report
EA  
LI   Level Indicator
Enforcement Action  
LOCA Loss of Coolant Accident
EC  
LOLC Loss of Level Control
Engineering Change  
LOOP Loss of Off-site Power
EDE  
LT   Level Transmitter
Effective Dose Equivalent  
mrem Millirem
ELHX  
MSPI Mitigating Systems Performance Index
Excess Letdown Heat Exchanger  
NCV   Non-Cited Violation
EP  
NEI   Nuclear Energy Institute
Emergency Preparedness  
NMC   Nuclear Management Company
EPRI  
NRC   U.S. Nuclear Regulatory Commission
Electric Power Research Institute  
NSCIT Nuclear Safety Culture Improvement Team
EPU  
OSHA Occupational Health and Safety Administration
Extended Power Up-Rate  
                                    18            Attachment
ERO  
Emergency Response Organization  
FPL  
Florida Power and Light  
FSAR  
Final Safety Analysis Report  
FW  
Feedwater  
GL  
Generic Letter  
GSI  
Generic Safety Issue  
I&C  
Instrumentation and Control  
IEL  
Initiating Event Likelihood  
IMC  
Inspection Manual Chapter  
IP  
Inspection Procedure  
IR  
Inspection Report  
ISI  
Inservice Inspection  
LER  
Licensee Event Report  
LI  
Level Indicator  
LOCA  
Loss of Coolant Accident  
LOLC  
Loss of Level Control  
LOOP  
Loss of Off-site Power  
LT  
Level Transmitter  
mrem  
Millirem  
MSPI  
Mitigating Systems Performance Index  
NCV  
Non-Cited Violation  
NEI  
Nuclear Energy Institute  
NMC  
Nuclear Management Company  
NRC  
U.S. Nuclear Regulatory Commission  
NSCIT  
Nuclear Safety Culture Improvement Team  
OSHA  
Occupational Health and Safety Administration  


P&ID Piping and Instrumentation Diagram
PARS Publicly Available Records System
19
PBNP Point Beach Nuclear Plant
Attachment
PI   Performance Indicator
P&ID  
POS Plant Operating State
Piping and Instrumentation Diagram  
PMT Post-Maintenance Testing
PARS  
PT   Pressure Test
Publicly Available Records System  
RCA Radiologically Controlled Area
PBNP  
RCS Reactor Coolant System
Point Beach Nuclear Plant  
RFO Refueling Outage
PI  
RHR Residual Heat Removal
Performance Indicator  
RWP Radiation Work Permit
POS  
RWST Refueling Water Storage Tank
Plant Operating State  
SCWE Safety-Conscious Work Environment
PMT  
SDP Significance Determination Process
Post-Maintenance Testing  
SG   Steam Generator
PT  
SI   Safety Injection
Pressure Test  
SLP Safe Load Path
RCA  
SQUG Seismic Qualification Users Group
Radiologically Controlled Area  
SRA Senior Reactor Analyst
RCS  
SW   Service Water
Reactor Coolant System  
TI   Temporary Instruction
RFO  
TS   Technical Specification
Refueling Outage  
TSAC Technical Specification Action Statement
RHR  
TTB Time-to-Boil
Residual Heat Removal  
URI Unresolved Item
RWP  
VT   Visual Examination
Radiation Work Permit  
WO   Work Order
RWST  
                                    19        Attachment
Refueling Water Storage Tank  
SCWE  
Safety-Conscious Work Environment  
SDP  
Significance Determination Process  
SG  
Steam Generator  
SI  
Safety Injection  
SLP  
Safe Load Path  
SQUG  
Seismic Qualification Users Group  
SRA  
Senior Reactor Analyst  
SW  
Service Water  
TI  
Temporary Instruction  
TS  
Technical Specification  
TSAC  
Technical Specification Action Statement  
TTB  
Time-to-Boil  
URI  
Unresolved Item  
VT  
Visual Examination  
WO  
Work Order  


L. Meyer                                             -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosure will be available electronically for public inspection in the NRC Public Document
L. Meyer  
Room or from the Publicly Available Records System (PARS) component of NRC's document
system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-
rm/adams.html (the Public Electronic Reading Room).
                                                    Sincerely,
                                                    /RA/
-2-  
                                                    Michael Kunowski, Chief
                                                    Branch 5
                                                    Division of Reactor Projects
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its  
Docket Nos. 50-266; 50-301
enclosure will be available electronically for public inspection in the NRC Public Document  
License Nos. DPR-24; DPR-27
Room or from the Publicly Available Records System (PARS) component of NRC's document  
Enclosure:         IR 05000266/2009005; 05000301/2009005
system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-
                    w/Attachment: Supplemental Information
rm/adams.html (the Public Electronic Reading Room).  
cc w/encl:         Distribution via ListServe
DOCUMENT NAME: G:\1-Secy\1-Work In Progress\POI 2009 005.doc
  Publicly Available           Non-Publicly Available       Sensitive   Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl
"E" = Copy with attach/encl "N" = No copy
OFFICE           RIII             RIII
  NAME             SOrth             MKunowski:cms
Sincerely,  
  DATE             02/10/2010       02/10/2010
                                          OFFICIAL RECORD COPY
/RA/  
Michael Kunowski, Chief  
Branch 5  
Division of Reactor Projects  
Docket Nos. 50-266; 50-301  
License Nos. DPR-24; DPR-27  
Enclosure:  
IR 05000266/2009005; 05000301/2009005
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServe  
DOCUMENT NAME: G:\\1-Secy\\1-Work In Progress\\POI 2009 005.doc  
  Publicly Available  
Non-Publicly Available  
Sensitive  
Non-Sensitive  
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl  
"E" = Copy with attach/encl "N" = No copy  
OFFICE  
RIII  
RIII  
 
   
NAME  
SOrth  
MKunowski:cms  
   
DATE  
02/10/2010  
02/10/2010  
OFFICIAL RECORD COPY  


Letter to L. Meyer from M. Kunowski dated February 10, 2010
SUBJECT:       POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED
              INSPECTION REPORT 05000266/2009005; 05000301/2009005 AND STATUS
Letter to L. Meyer from M. Kunowski dated February 10, 2010  
              OF CONFIRMATORY ORDER EA-06-178
DISTRIBUTION:
SUBJECT:  
Susan Bagley
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED  
RidsNrrDorlLpl3-1 Resource
INSPECTION REPORT 05000266/2009005; 05000301/2009005 AND STATUS  
RidsNrrPMPointBeach
OF CONFIRMATORY ORDER EA-06-178  
RidsNrrDirsIrib Resource
DISTRIBUTION:  
Cynthia Pederson
Susan Bagley  
Steven Orth
RidsNrrDorlLpl3-1 Resource  
Jared Heck
RidsNrrPMPointBeach  
Allan Barker
RidsNrrDirsIrib Resource  
Carole Ariano
Cynthia Pederson
Linda Linn
Steven Orth  
DRPIII
Jared Heck  
DRSIII
Allan Barker  
Patricia Buckley
Carole Ariano  
Tammy Tomczak
Linda Linn  
DRPIII  
DRSIII  
Patricia Buckley  
Tammy Tomczak  
ROPreports Resource
ROPreports Resource
}}
}}

Latest revision as of 06:39, 14 January 2025

IR 05000266-09-005, 05000301-09-005, on 10/01/2009 - 12/31/2009, Point Beach Nuclear Plant, Units 1 & 2, Maintenance Effectiveness, Operability Evaluations, Plant Modifications, Outage Activities, and Other Activities
ML100410106
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 02/10/2010
From: Michael Kunowski
NRC/RGN-II/DRP/RPB5
To: Meyer L
Point Beach
References
EA-06-178 IR-09-005
Download: ML100410106 (78)


See also: IR 05000266/2009005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

February 10, 2010

EA-06-178

Mr. Larry Meyer

Site Vice-President

NextEra Energy Point Beach, LLC

6610 Nuclear Road

Two Rivers, WI 54241

SUBJECT:

POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED

INSPECTION REPORT 05000266/2009005; 05000301/2009005 AND STATUS

OF CONFIRMATORY ORDER EA-06-178

Dear Mr. Meyer:

On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a baseline

inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed report documents

the inspection results, which were discussed on January 6, 2010, with Mr. C. Trezise and

members of your staff. The report also documents the status of Confirmatory Order EA-06-178,

as it relates to your Point Beach Nuclear Plant.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commission's rules and regulations, and with the conditions of your

license. The inspectors reviewed selected procedures and records, observed activities, and

interviewed your personnel.

Based on the results of this inspection, two NRC-identified and three self-revealed findings of

very low safety significance were identified. Of these findings, four involved a violation of

NRC requirements. However, because of their very low safety significance, and because the

issues were entered into your corrective action program, the NRC is treating these issues as

Non-Cited Violations (NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy.

If you contest the subject or severity of these NCVs, you should provide a response within

30 days of the date of this Inspection Report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001,

with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Point Beach Nuclear Plant. In addition, if you disagree with the characterization of

any finding in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your disagreement, to the Regional Administrator,

Region III, and the NRC Resident Inspector Office at the Point Beach Nuclear Plant.

The information that you provide will be considered in accordance with Inspection Manual

Chapter 0305.

L. Meyer

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records System (PARS) component of NRC's document

system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Michael Kunowski, Chief

Branch 5

Division of Reactor Projects

Docket Nos. 50-266; 50-301

License Nos. DPR-24; DPR-27

Enclosure:

IR 05000266/2009005; 05000301/2009005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServe

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-266; 50-301

License Nos:

DPR-24; DPR-27

Report No:

05000266/2009005; 05000301/2009005

Licensee:

NextEra Energy Point Beach, LLC

Facility:

Point Beach Nuclear Plant, Units 1 and 2

Location:

Two Rivers, WI

Dates:

October 1, 2009, through December 31, 2009

Inspectors:

S. Burton, Senior Resident Inspector

R. Ruiz, Senior Resident Inspector (Acting)

M. Thorpe-Kavanaugh, Resident Inspector (Acting)

J. Jandovitz, Project Engineer

J. Cassidy, Senior Health Physicist

`

R. Jickling, Senior Emergency Preparedness Inspector

D. Jones, Reactor Inspector

D. McNeil, Senior Operations Engineer

R. Edwards, Reactor Engineer

J. Gilliam, Reactor Engineer

E. Sanchez-Santiago, Reactor Engineer

N. Feliz Adorno, Reactor Engineer

Approved by:

M. Kunowski, Chief

Branch 5

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ...........................................................................................................1

REPORT DETAILS.......................................................................................................................5

Summary of Plant Status...........................................................................................................5

1.

REACTOR SAFETY .......................................................................................................5

1R01

Adverse Weather Protection (71111.01) .............................................................5

1R04

Equipment Alignment (71111.04) ........................................................................5

1R05

Fire Protection (71111.05) ...................................................................................7

1R06

Flooding (71111.06).............................................................................................8

1R08

Inservice Inspection (ISI) Activities (71111.08P) .................................................8

1R11

Licensed Operator Requalification Program (71111.11)....................................11

1R12

Maintenance Effectiveness (71111.12) .............................................................13

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)........16

1R15

Operability Evaluations (71111.15)....................................................................16

1R18

Plant Modifications (71111.18) ..........................................................................20

1R19

Post-Maintenance Testing (71111.19)...............................................................25

1R20

Outage Activities (71111.20) .............................................................................26

1R22

Surveillance Testing (71111.22) ........................................................................29

1EP2

Alert and Notification System (ANS) Evaluation (71114.02)..............................30

1EP3

Emergency Response Organization Augmentation Testing (71114.03)............30

1EP4

Emergency Action Level and Emergency Plan Changes (71114.04)................31

1EP5

Correction of EP Weaknesses and Deficiencies (71114.05) .............................31

2.

RADIATION SAFETY ...................................................................................................32

2OS1

Access Control to Radiologically Significant Areas (71121.01) .........................32

2OS2

ALARA Planning and Controls (71121.02) ........................................................37

4.

OTHER ACTIVITIES ....................................................................................................38

4OA1

PI Verification (71151) .......................................................................................38

4OA2

Identification and Resolution of Problems (71152) ............................................41

4OA5

Other Activities...................................................................................................43

4OA6

Management Meetings ......................................................................................53

SUPPLEMENTAL INFORMATION ...............................................................................................1

Key Points of Contact................................................................................................................1

List of Items Opened, Closed and Discussed ...........................................................................1

List of Documents Reviewed.....................................................................................................3

List of Acronyms Used ............................................................................................................18

Enclosure

1

SUMMARY OF FINDINGS

IR 05000266/2009005, 05000301/2009005; 10/01/2009 - 12/31/2009; Point Beach Nuclear

Plant, Units 1 & 2; Maintenance Effectiveness, Operability Evaluations, Plant Modifications,

Outage Activities, and Other Activities.

This report covers a three-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Also discussed is the status of Confirmatory Order

EA-06-178. Five Green findings were either self-revealed or identified by inspectors in this

inspection period. Four of the findings had associated Non-Cited Violations of

NRC requirements, and one finding had no associated violation of regulatory requirements.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP).

Findings for which the SDP does not apply may be Green or be assigned a severity level after

NRC management review. The NRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4,

dated December 2006.

A.

NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a finding of very low safety significance for the failure to

meet a commitment made in the Generic Letter (GL) 89-13 program. Specifically, the

program states that biocide treatments at Point Beach are performed at least annually

and are directly applied to the service water system for mussel control and eradication to

prevent fouling of safety-related heat exchangers. However, the 2008 biocide treatment

for mussel control was deferred until 2009. After the treatment in 2009, greater than

expected tube blockage and reduced flow to safety-related heat exchangers due to

mussels was identified. In response, the licensee adjusted flow through the affected

heat exchangers and opened and cleaned the heat exchangers to remove mussels that

caused the tube blockage. The licensee took corrective actions to ensure that future

annual biocide treatments would be conducted annually.

This finding was more than minor because it was associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and adversely affected the

associated cornerstone objective of ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. The

inspectors determined the finding could be evaluated using the SDP in accordance with

IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial

Screening and Characterization of Findings," Table 4a, for the Mitigating Systems

Cornerstone, dated January 10, 2008. The finding was determined to be of very low

safety significance because the issue did not result in the actual loss of a safety function.

This finding did not involve a violation of NRC regulatory requirements. The inspectors

determined this performance deficiency was not indicative of current performance;

therefore, no cross-cutting aspect was identified. (Section 1R12.1)

Green. The inspectors identified a finding of very low safety significance and associated

Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the

failure to update the Safe Load Path Manual for the Unit 2 turbine building (SLP-3) as

part of the mid-1990's modification that added the G-03 and G-04 emergency diesel

Enclosure

2

generators. Specifically, it was identified that SLP-3 allowed unrestricted load lifts over

the Unit 2 turbine building truck bay area based upon a 1980's evaluation, and was not

updated to reflect a modification that added safety-related cables for emergency diesel

generators under the Unit 2 truck bay. Due to the close proximity of the A train cables

to the B train cables, a loss of both trains of emergency alternating current (AC) power

could result if the underground cables were disabled by a dropped load of sufficient

magnitude. The licensee addressed the immediate concern by installing temporary steel

plates over the affected area of the truck bay to provide adequate protection for

upcoming heavy load lifts. Additionally, the licensee revised SLP-3 to require additional

risk mitigation measures be taken prior to heavy load lifts in that area.

The finding was more than minor because it was associated with the Mitigating Systems

Cornerstone attribute of design control and adversely affected the associated

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences

(i.e., core damage). The inspectors determined the finding could be evaluated using

the SDP in accordance with IMC 0609, "Significance Determination Process,"

Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings,"

Table 4a, for the Mitigating Systems Cornerstone, dated January 10, 2008. The finding

was determined to be of very low safety significance because the issue did not result in

the actual loss of a safety function. This finding had a cross-cutting aspect in the area of

problem identification and resolution, corrective action program component, because the

staff did not take appropriate corrective actions to address safety issues in a timely

manner, commensurate with their safety significance. Specifically, in 2008, when

questions were raised by licensee staff regarding the adequacy of SLP-3, the SLP was

not revised (P.1(d)). (Section 1R18.1)

Green. A self-revealed finding of very low safety significance and associated Non-Cited

Violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and

Drawings," was identified for performing an Instrumentation and Control (I&C) procedure

that was inappropriate to the circumstances, and resulted in the momentary loss of all

available channels of reactor vessel level indication in the control room. As part of the

immediate corrective actions, the licensee suspended the performance of the procedure

and sent an operator into containment to verify reactor vessel level via the local

standpipe level indicator and to ensure level indication was reestablished. Additionally,

the licensee applied a work planning logic-tie to this activity to ensure the reactor was

de-fueled prior to performing this calibration and was currently evaluating the need for

revisions to the procedure.

The finding was more than minor because it was associated with the Mitigating Systems

Cornerstone attribute of procedure quality and adversely affected the associated

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core damage).

The inspectors assessed the significance of the finding in accordance with IMC 0609,

Appendix G, "Shutdown Operations Significance Determination Process," and

determined that this issue required a Phase 2 analysis since the finding increased the

likelihood of a loss of reactor coolant system inventory. The inspectors and a senior

reactor analyst determined through the analysis that this issue is best characterized as a

finding of very low safety significance. This finding had a cross-cutting aspect in the

area of human performance, work control component, in that the licensee did not

appropriately coordinate work activities for the existing plant conditions to ensure the

Enclosure

3

operational impact on reactor vessel level indication while at a water level above

reduced inventory was fully understood (H.3(b)). (Section 1R20.1)

Cornerstone: Barrier Integrity

Green. A self-revealed finding of very low safety significance and associated Non-Cited

Violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and

Drawings," was identified for the failure to ensure adequate control of foreign material in

accordance with the requirements of procedure NP 8.4.10, "Exclusion of Foreign

Material from Plant Components and Systems." Specifically, on October 17, 2009,

foreign material was discovered inside the 2SI-897B valve after the valve failed to

properly stroke during the performance of procedure IT-215, "SI Valves -

Cold Shutdown." The licensee took prompt corrective actions to repair the valve and

perform an extent-of-condition review. Additionally, upon entering the issue into its

corrective action program, the licensee performed a causal evaluation to determine any

additional corrective actions.

The finding was more than minor because it was associated with the Barrier Integrity

Cornerstone attribute of human performance and adversely affected the associated

cornerstone objective of providing reasonable assurance that physical design barriers

protect the public from radionuclide releases caused by accidents or events.

Specifically, due to the interference caused by the foreign material inside the 2SI-897B

valve, the valve would not have been able to perform its safety function to close during

the initiation of the post-LOCA (loss of coolant accident) sump-recirculation phase of

safety injection. The inspectors determined the finding could be evaluated in

accordance with IMC 0609, Significance Determination Process," Attachment 0609.04,

Phase 1 - Initial Screening and Characterization of Findings," Table 4a, dated

January 10, 2008. The finding was determined to be of very low safety significance

because the issue did not represent a degradation of the radiological barrier function

provided for the control room, the auxiliary building, or the spent fuel pool; represent a

degradation of the barrier function of the control room against smoke or a toxic

atmosphere; represent an actual open pathway in the physical integrity of reactor

containment (valves, airlocks, containment isolation system (logic and instrumentation)),

and heat removal components; or involve an actual reduction in function of hydrogen

ignitors in the reactor containment. No cross-cutting aspect was identified because the

foreign material was determined to have been introduced into the system in the past and

was not considered indicative of current performance. (Section 1R15.1)

Cornerstone: Public Radiation Safety

Green. A self-revealed finding of very low safety significance and associated Non-Cited

Violation of 10 CFR 20.1101(b) was identified for the failure to adequately control

radioactive material to prevent its migration outside the radiologically controlled area

(RCA), as required by licensee procedures. On May 21, 2009, a contract worker

performing inspections of the main electrical transformers located outside the RCA

picked-up a wadded-ball of debris (unmarked tape) and placed it in his front pants

pocket. The debris was later found to be radioactively contaminated when the worker

alarmed the protected area exit radiation monitors a few hours later as he attempted to

leave the site. The tape was likely used to cover contaminated hoses that were

previously used within the Point Beach RCA, but had escaped the licensee's control and

migrated (blew) into the transformer area outdoors where it was found by the worker.

Enclosure

4

The licensee's storage of radioactive material in an outdoor satellite RCA and/or the

licensee's radioactive material control practices during refueling outages when the

containment building equipment hatch was open to the environment led to the escape of

the material outside the RCA. The contractor's assigned work duties should not have

involved exposure to radioactive material; consequently, the worker was unnecessarily

exposed to radiation from the contaminated tape. A dose evaluation completed by the

licensee's consultant determined that the effective dose equivalent to the worker's thigh

from exposure to the contaminated ball of tape was approximately one mrem.

The licensee's corrective action called for expanded radiation protection oversight during

movement of material in outdoor areas. Procedures were revised to include a

post-outage walkdown of outdoor areas near the RCA yard. Additionally, the licensee

planned to construct an enclosure so that storage/transfer of contaminated materials

could be performed indoors.

The finding was more than minor because it impacted the program and process attribute

of the Public Radiation Safety Cornerstone and adversely affected the cornerstone

objective of ensuring adequate protection of public health and safety from exposure to

radiation, in that, unnecessary radiation exposure was received by an individual from

inadequately controlled radioactive material. The finding was determined to be of very

low safety significance because: (1) it involved a radioactive material control problem

that was contrary to NRC requirements and the licensee's procedure; and (2) the dose

impact to a member of the public (the contract worker) within the licensee's restricted

area was less than 5 millirem total effective dose equivalent. The cause of the

radioactive material control problem involved a cross-cutting component in the human

performance area for inadequate work control, in that, job site conditions including

environmental conditions (high winds, night time work, etc.) impacted human

performance and consequently, radiological safety, during movement of

material/equipment in outdoor areas (H.3.(a)). (Section 4OA5.1)

B.

Licensee-Identified Violations

None.

Enclosure

5

REPORT DETAILS

Summary of Plant Status

Unit 1 was at 100 percent power throughout the entire inspection period with the exception of a

planned reduction in power during routine auxiliary feedwater (AFW) testing and an unplanned

down-power to approximately 45 percent power on November 17, 2009, due to a lake grass

influx and subsequent condenser cleaning evolution.

Unit 2 was at 100 percent power at the beginning of the inspection period, shut down to

commence a refueling outage (U2R30) on October 15, 2009, restarted on December 5, and

returned to 100 percent power on December 11. Unit 2 remained at or near 100 percent power

for the remainder of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1

Winter Seasonal Readiness Preparations

a.

Inspection Scope

The inspectors conducted a review of the licensees preparations for winter to verify that

the plants design features and implementation of procedures were sufficient to protect

mitigating systems from the effects of adverse weather. The inspectors walked down

accessible portions of risk-significant equipment and systems susceptible to cold

weather freezing prior to the onset of severe cold weather. The inspectors walked down

all accessible portions of the Units 1 and 2 facade buildings, which enclosed the reactor

containments, and certain safety-related plant equipment inside the protected area. The

inspectors reviewed the corrective action documents and work orders (WOs) written for

identified problems. The inspectors also walked down areas that had a history of freeze

problems to ensure that previous corrective actions were implemented. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b.

Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a.

Inspection Scope

The inspectors performed a partial system walkdown of the spent fuel pool cooling

system.

Enclosure

6

The inspectors selected this system based on its risk significance relative to the Reactor

Safety Cornerstones at the time it was inspected. The inspectors attempted to identify

any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Final Safety Analysis Report (FSAR), Technical Specification (TS)

requirements, outstanding WOs, condition reports, and the impact of ongoing work

activities on redundant trains of equipment in order to identify conditions that could have

rendered the systems incapable of performing their intended functions. The inspectors

also walked down accessible portions of the system to verify system components and

support equipment were aligned correctly and operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the corrective action program (CAP) with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

These activities constituted one partial system walkdown sample as defined in

IP 71111.04-05.

b.

Findings

No findings of significance were identified.

.2

Semi-Annual Complete System Walkdown

a.

Inspection Scope

During the Unit 2 refueling outage (U2R30), the inspectors performed a complete system

alignment inspection of the residual heat removal (RHR) system to verify the functional

capability of the system. This system was selected because it was considered both

safety-significant and risk-significant in the licensee's probabilistic risk assessment.

The inspectors walked down the system to review mechanical and electrical equipment

lineups, electrical power availability, system pressure and temperature indications, as

appropriate, component labeling, component lubrication, component and equipment

cooling, hangers and supports, operability of support systems, and to ensure that

ancillary equipment or debris did not interfere with equipment operation. A review of a

sample of past and outstanding WOs was performed to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the CAP database to ensure that system equipment alignment problems were

being identified and appropriately resolved. Documents reviewed are listed in the

Attachment to this report.

These activities constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b.

Findings

No findings of significance were identified.

Enclosure

7

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

fire zone 245 - Unit 1 electrical equipment room;

fire zone 318 - cable spreading room;

fire zone 775 - G-04 emergency diesel generator (EDG); and

fire zone 301 - Unit 2 turbine building basement.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded, or inoperable fire protection

equipment, systems, or features in accordance with the licensee's fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

and their potential to impact equipment that could initiate or mitigate a plant transient.

The inspectors verified that fire hoses and extinguishers were in their designated

locations and available for immediate use; fire detectors and sprinklers were

unobstructed; transient material loading was within the analyzed limits; and fire doors,

dampers, and penetration seals appeared to be in satisfactory condition. The inspectors

also verified that minor issues identified during the inspection were entered into the

licensee's CAP. Documents reviewed are listed in the Attachment to this report.

These activities constituted four quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b.

Findings

No findings of significance were identified.

.2

Annual Fire Protection Drill Observation (71111.05A)

a.

Inspection Scope

On December 10, 2009, the inspectors observed a fire brigade activation in the north

service building in response to a simulated electrical fire in the warehouse storeroom.

Based on this observation, the inspectors completed an annual evaluation of the

readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee

staff identified deficiencies, openly discussed them in a self-critical manner at the drill

debrief, and took appropriate corrective actions. Specific attributes evaluated were:

(1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper

use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;

(4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade

leader communications, command, and control; (6) search for victims and propagation of

Enclosure

8

the fire into other plant areas; (7) smoke removal operations; (8) utilization of

pre-planned strategies; (9) adherence to the pre-planned drill scenario; and

(10) drill objectives. Documents reviewed are listed in the Attachment to this report.

These activities constituted one annual fire protection inspection sample as defined in

IP 71111.05-05.

b.

Findings

No findings of significance were identified.

1R06 Flooding (71111.06)

.1

Internal Flooding

a.

Inspection Scope

The inspectors reviewed selected important-to-safety plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the FSAR, engineering calculations, and abnormal operating procedures to

identify licensee commitments. In addition, the inspectors reviewed licensee drawings to

identify areas and equipment that may be affected by internal flooding caused by the

failure or misalignment of nearby sources of water, such as the fire suppression or the

circulating water systems. The inspectors also reviewed the licensee's corrective action

documents with respect to past flood-related items identified in the CAP to verify the

adequacy of the corrective actions. The inspectors performed a walkdown of the

following plant area to assess the adequacy of flood protection and mitigation features,

verify drains and sumps were clear of debris and were functional, and verify that the

licensee complied with its commitments. Documents reviewed are listed in the

Attachment to this report.

G-01 and G-02 EDG rooms.

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b.

Findings

No findings of significance were identified.

1R08 Inservice Inspection (ISI) Activities (71111.08P)

From November 2 through November 6, 2009, the inspectors conducted a review of the

implementation of the licensee's ISI program for monitoring degradation of the reactor

coolant system (RCS), steam generator (SG) tubes, AFW systems, risk-significant piping

and components, and containment systems.

The inspections described in Sections 1R08.1, 1R08.2, 1R08.3, 1R08.4, and 1R08.5

below constituted one ISI sample as defined in IP 71111.08-05.

Enclosure

9

.1

Piping Systems ISI

a. Inspection Scope

The inspectors observed and reviewed records of the following nondestructive

examinations mandated by the American Society of Mechanical Engineers (ASME)

Section XI Code to evaluate compliance with the ASME Code Section XI and Section V

requirements and if any indications and defects detected were detected, and to

determine if these were dispositioned in accordance with the ASME Code or an

NRC-approved alternative requirement.

ultrasonic examination of steam generator shell-to-head circumferential weld

SG-A-5R1 (Report No. 2009UT-22);

liquid penetrant examination of reactor closure head peripheral control rod drive

mechanism housings 28 and 32 welds (Report No. 2009PT-001); and

ultrasonic examination of the reactor coolant system pressurizer surge nozzle

inside radius section weld (Report No. 2009UT-057).

The inspectors reviewed records of the following nondestructive examinations conducted

as part of the licensee's industry initiative inspection program for primary water stress

corrosion cracking to determine if the examinations were conducted in accordance with

the licensee's augmented inspection program, industry guidance documents, and

associated licensee examination procedures, and if any indications and defects were

detected, to determine if these were dispositioned in accordance with approved

procedures and NRC requirements.

visual examination of SG outlet nozzle-to-safe end weld RC-36-MRCL-AII-01A

(Report No. 2009VT-031);

visual examination of SG safe-end to "A" S/G inlet nozzle weld

RC-34-MRCL-AI-05 (Report No. 2009VT-030);

visual examination of SG "A" cold leg vent nozzle, (Report No. 2009VT-029); and

visual examination of SG "A" hot leg vent nozzle, (Report No. 2009VT-028).

There were no examinations completed during the previous outage with relevant or

recordable conditions or indications accepted for continued service. Therefore, no

NRC review was completed for this inspection procedure attribute.

The inspectors reviewed the following pressure boundary weld repairs completed on

risk-significant systems since the beginning of the last refueling outage (RFO) to verify

that the welding and any associated non-destructive examinations were performed in

accordance with the Construction Code and ASME Code,Section XI. Additionally, the

inspectors reviewed the welding procedure specification and supporting weld procedure

qualification records to determine if the weld procedure(s) were qualified in accordance

with the requirements of Construction Code and the ASME Section IX Code.

Work Order 00352831, Replacement of an ASME Section III, Class 1,

Excess Letdown Heat Exchanger (ELHX) 2HX-4 Outlet Drain Valve 2CV-D-11;

and

Work Order 00352519, Replacement of an ASME Section III, Class 1, RCS to

P-10A/B Residual Heat Removal (RHR) Pump Suction Header Drain

Valve 2RH-D-9.

Enclosure

10

b. Findings

No findings of significance were identified.

.2

Reactor Pressure Vessel Upper Head Penetration Inspection Activities

a.

Inspection Scope

For the Unit 2 reactor vessel head, a bare metal visual examination was required this

outage pursuant to 10 CFR 50.55a(g)(6)(ii)(D).

The inspectors reviewed records of the visual examination conducted on the Unit 2

reactor vessel head at penetrations 16, 32, and 40 to determine if the activities were

conducted in accordance with the requirements of ASME Code Case N-729-1 and

10 CFR 50.55a(g)(6)(ii)(D). In particular, the inspectors confirmed that:

the required visual examination scope/coverage was achieved in accordance

with the licensee's procedures; and

the criteria for visual examination quality and instructions for resolving

interference and masking issues were adequate.

No indications of potential through-wall leakage were identified by the licensee.

Therefore, no NRC review was completed for this IP attribute.

The licensee did not perform any welded repairs to vessel head penetrations since the

beginning of the preceding outage for Unit 2. Therefore, no NRC review was completed

for this IP attribute.

b.

Findings

No findings of significance were identified.

.3

Boric Acid Corrosion Control (BACC)

a. Inspection Scope

The inspectors observed and reviewed records of the licensee's initial BACC visual

examinations and verified whether these visual examinations emphasized locations

where boric acid leaks could cause degradation of safety-significant components.

The inspectors reviewed the following licensee evaluations of RCS components with

boric acid deposits to determine if degraded components were documented in the CAP.

The inspectors also evaluated corrective actions for any degraded RCS components to

determine if they met the component Construction Code, ASME Section XI Code, and/or

NRC-approved alternative.

boric acid evaluation No.09-219, 2SC-953 boric acid indications; and

boric acid evaluation No. 09-173B, 2P-116, 2T-6C BA tank recirculation pump.

The inspectors reviewed the following corrective actions related to evidence of boric acid

leakage to determine if the corrective actions completed were consistent with the

Enclosure

11

requirements of the ASME Section XI Code and 10 CFR Part 50, Appendix B,

Criterion XVI.

Work Order Package 0035658301, Replace Pump Mechanical Seal; and

Work Request No. 00039792, Adjust Packing to Last Value During AOV

[air operated valve] Diagnostics.

b. Findings

No findings of significance were identified.

.4

Steam Generator Tube Inspection Activities

a. Inspection Scope

For the Unit 2 SGs, no examination was required pursuant to the TSs during the current

RFO, U2R30. Therefore, no NRC review was completed for this IP attribute.

b. Findings

No findings of significance were identified.

.5

Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI/SG-related problems entered into the

licensee's CAP and conducted interviews with licensee staff to determine if:

the licensee had established an appropriate threshold for identifying

ISI/SG-related problems;

the licensee had taken appropriate corrective actions; and

the licensee had evaluated operating experience and industry generic issues

related to ISI and pressure boundary integrity.

The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, "Corrective Action," requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1

Resident Inspector Quarterly Review (71111.11Q)

a.

Inspection Scope

On December 1, 2009, the inspectors observed a crew of licensed operators in the

plant's simulator during just-in-time training for the Unit 2 startup to verify that operator

Enclosure

12

performance was adequate, evaluators were identifying and documenting crew

performance problems, and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

licensed operator performance;

crew's clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crew's performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b.

Findings

No findings of significance were identified.

.2

Annual Operating Test Results (71111.11B)

a.

Inspection Scope

The inspectors reviewed the overall pass/fail results of the individual Job Performance

Measure operating tests, and the simulator operating tests (required to be given

per 10 CFR 55.59(a)(2)) administered by the licensee from August 10 through

October 1, 2009, as part of the licensee's operator licensing requalification cycle.

These results were compared to the thresholds established in IMC 0609, Appendix I,

"Licensed Operator Requalification Significance Determination Process."

The evaluations were also performed to determine if the licensee effectively

implemented operator requalification guidelines established in NUREG 1021,

"Operator Licensing Examination Standards for Power Reactors," and IP 71111.11,

"Licensed Operator Requalification Program." Documents reviewed are listed in the

Attachment to this report.

Completion of this section constituted one biennial licensed operator requalification

inspection sample as defined in IP 71111.11B.

b.

Findings

No findings of significance were identified.

Enclosure

13

1R12 Maintenance Effectiveness (71111.12)

.1

Containment Accident Fan Cooler Units (71111.12Q)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant system:

containment accident fan cooler units.

The inspectors reviewed events, such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems, and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

verifying appropriate performance criteria for structures, systems, and

components/functions classified as (a)(2) or appropriate and adequate goals and

corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly maintenance effectiveness sample as defined

in IP 71111.12-05.

b.

Findings

Failure to Meet Generic Letter (GL) 89-13 Program for Mussel Control

Introduction: The inspectors identified a Green finding for the failure to meet a

GL 89-13, "Service Water System Problems Affecting Safety-Related Equipment,"

program commitment. Specifically, the licensee committed to implement mussel control

methods to prevent fouling of safety-related heat exchangers. The 2008 annual biocide

treatment for mussel control was not conducted and excessive tube blockage and

reduced flow to safety-related heat exchangers due to mussels was identified after

treatment in 2009.

Description: In response to GL 89-13, Point Beach developed a program documenting

GL 89-13 commitments made to the NRC. Among those commitments was one to

implement a biofouling program for mussel control and eradication to prevent fouling of

safety-related components.

Enclosure

14

In 1999, the plant experienced significant mussel blockage events after not performing a

biocide treatment in the previous year. In 2000, a licensee review of the mussel control

strategy determined that two biocide treatments per year should be implemented so that

mussels did not grow to a size that would block heat exchanger tubes when the shells

detach from the piping. However, since that time, the plant performed only one biocide

treatment per year, which empirically appeared adequate.

In August 2008, the annual mussel biocide treatment was deferred due to concerns by

operations that the treatment would impact the operation of safety-related components.

The decision, however, was made without consulting the GL 89-13 program engineer or

the service water (SW) system engineer. It was possible to defer the treatment with

minimal reviews since the WO was inappropriately categorized as a low Priority 4,

"other," task.

The missed biocide treatment was documented in the CAP as Action Request (AR)

1133110, and corrective actions were implemented. None of the corrective actions

discussed rescheduling the biocide treatment in 2008. Instead, the decision was made

to perform the SW system biocide treatments for Unit 1 in spring and fall 2009, and for

Unit 2 in fall 2009, just prior to the RFO. This schedule resulted in the Unit 2 SW system

not being treated for about two years.

The Unit 2 mussel biocide treatment was completed on October 8, 2009. The following

day, Unit 2 entered an unexpected Technical Specification Action Condition (TSAC) due

to low flow in containment fan cooler (CFC) 2HX-15D. Flow was promptly increased by

operations, and the TSAC was exited. Subsequently, during the Unit 2 outage (within a

month of the biocide treatment) the component cooling water heat exchangers

(CCWHXs), 2HX-12D and 0HX-12C (those affected by the Unit 2 biocide treatment), and

the Unit 2 CFCs, 2HX-15A, 2HX-15C, and 2HX-15D, were opened for inspection.

The CCWHXs acceptance criterion for the number of tubes blocked was 160 tubes.

In 2HX-12D, 828 tubes were found blocked and in 0HX-12C, 507 tubes were blocked by

mussel shells. The CFCs acceptance criterion for blocked tubes is 25 tubes. The plant

identified 46, 107, and 77 tubes blocked by mussel shells in 2HX-15A, 2HX-15C, and

2HX-15D respectively. The 2HX-15B CFC was found acceptable. All heat exchangers

were cleaned and mussel shells removed from the tubes. The inspectors reviewed the

licensees evaluation of past operability for the unacceptable CCWHXs, which concluded

they had been operable during power operations, and found no issues.

Analysis: The inspectors determined that the failure to prevent fouling of safety-related

heat exchangers in accordance with GL 89-13 commitments was a performance

deficiency. Specifically, the deferral of the 2008 biocide treatment allowed mussels to

grow to sufficient size that they would no longer pass through the heat exchanger tubes

and the licensee could have reasonably been expected to prevent this based on past

experience. The finding was determined to be more than minor because the finding was

associated with the Mitigating Systems Cornerstone attribute of equipment performance

and adversely affected the associated cornerstone objective of ensuring the reliability

and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the failure to perform the 2008 biocide treatment affected

the operability and design requirements of the CCWHXs and the CFCs.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, "Significance Determination Process," Attachment 0609.04,

Enclosure

15

"Phase 1 - Initial Screening and Characterization of Findings," Table 4a, for the

Mitigating Systems Cornerstone, dated January 10, 2008. The finding was determined

to be of very low safety significance (Green) because the issue did not result in the

actual loss of a safety function or loss of a single train for greater than its allowed

TS time, and did not screen as potentially risk-significant due to seismic, flooding, or

severe weather initiating events. The inspectors determined this performance deficiency

was not indicative of current performance and therefore no cross-cutting issue was

identified.

Enforcement: No violation of regulatory requirements occurred because this issue

represents a failure to implement an NRC commitment. This finding was entered into

the licensee's CAP as AR 01158115 (FIN 05000266/2009005-01; 05000301/2009005-01).

In response to this issue, the licensee adjusted flow through the affected heat

exchangers to address the immediate low flow conditions in addition to opening and

cleaning all affected heat exchangers to remove mussel shells. In addition, the licensee

raised the priority of future annual biocide treatments by designating them as preventive

maintenance tasks. This re-designation will require more extensive reviews and

approvals if a plan to defer an annual treatment arises.

.2

Routine Quarterly Evaluations (71111.12Q)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant system:

gas turbine system.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

verifying appropriate performance criteria for structures, systems, and

components/functions classified as (a)(2) or appropriate and adequate goals and

corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

Enclosure

16

This inspection constituted one quarterly maintenance effectiveness sample as defined

in IP 71111.12-05.

b.

Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1

Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

week of November 16, 2009, following the circulating water grass intrusion event

and inverter trouble.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted

one sample as defined in IP 71111.13-05.

b.

Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1

Valve 2SI-897B Failure to Operate

a.

Inspection Scope

The inspectors reviewed AR 01158812, written due to the failure of the 2SI-897B valve

to operate during test procedure IT 215, "SI Valves - Cold Shutdown."

The inspectors selected this potential operability issue based on the risk significance of

the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS past-operability and system functionality

Enclosure

17

were properly justified and the subject component or system remained available such

that no unrecognized increase in risk occurred. The inspectors compared the operability

and design criteria in the appropriate sections of the TSs and FSAR to the licensee's

evaluations to determine whether the components or systems were operable or

functional. The inspectors determined, where appropriate, compliance with bounding

limitations associated with the evaluations. Additionally, the inspectors also reviewed a

sampling of corrective action documents to verify that the licensee was identifying and

correcting any deficiencies associated with operability evaluations. Documents reviewed

are listed in the Attachment to this report.

This operability inspection constituted one sample as defined in IP 71111.15-05.

b.

Findings

Failure to Ensure Adequate Control of Foreign Material in Safety-Related Systems

Introduction: A self-revealed finding of very low safety significance (Green) and

associated Non-Cited Violation (NCV) of 10 CFR Part 50, Appendix B, Criterion V,

"Instructions, Procedures and Drawings," was identified for the failure to ensure

adequate control of foreign material in accordance with the requirements of procedure

NP 8.4.10, "Exclusion of Foreign Material from Plant Components and Systems."

Description: On October 17, 2009, foreign material was discovered inside the 2SI-897B

valve after the valve failed to properly stroke closed during the performance of test

procedure IT-215, "SI Valves - Cold Shutdown." Due to the tight clearances in the valve

internals, once the foreign material became lodged in the valve trim cage, the valve plug

became stuck while it was being stroked. Upon retrieval of the material by the licensee,

it was discovered to be a pliable, black nylon material about 1/2-inch wide by 5-inches

long, and appeared to be a cable-tie of unknown origin or variety. The licensee

performed a boroscope inspection of the upstream and downstream piping for additional

fragments of the material and none were found. The licensee performed a Condition

Evaluation, AR 01158812, to determine the most likely source of the material.

The licensee concluded that the material most likely was introduced into the Unit 2

refueling water storage tank (RWST) where it flowed through a single-stage containment

spray pump during testing to the safety injection (SI) pump test recirculation line.

The licensee also concluded that due to the pliable nature of the material, it was highly

unlikely that the material would have damaged any pumps in its possible flow path.

Valve 2SI-897B is one of two normally-open, redundant, AOVs in series with valve

2SI-897A on the common Unit 2 SI pumps' test recirculation line (minimum-flow) to the

RWST. Together, these normally-open valves perform the safety function to remain

open during the SI injection phase to provide a minimum flow recirculation path to

prevent damage to the SI pumps as a result of operating in a low flow or dead-headed

condition. Since these valves were open, as designed, during modes in which the

SI system was required to be operable, this safety-function, and the operability of the

SI pumps was not impacted by this foreign material event.

The SI-897A and B valves also have a safety function to manually close during the

transition from the injection phase of SI to the sump recirculation phase to prevent the

flow of recirculation coolant into the RWST and potentially release radioactivity via the

RWST's open vent. During a small-break loss of coolant accident scenario, the

Enclosure

18

RHR pumps would take suction from the containment sump during the recirculation

phase and may be required to supply the SI pumps. If both SI-897A and B could not

close at that time, containment sump water would be lost to the RWST via the

minimum-flow line from the SI pumps, and radioactivity could be released to

atmosphere. It was this safety function that was affected when the foreign material

caused the mechanical binding of the 2SI-897B valve's internals and caused the valve to

bind when 75 percent shut during the performance of IT-215 on October 17. However,

since the 2SI-897A valve stroked satisfactorily on October 17, the safety function was

maintained by this redundant valve. The last time that the 2SI-897B valve was

successfully stroked was May 3, 2008, during the previous performance of IT-215.

Additionally, once these valves are required to shut during an accident scenario, there

are no sequences in which the valves would be required to re-open.

Analysis: The inspectors determined that the failure to ensure adequate control of

foreign material in safety-related systems was contrary to the requirements of

procedure NP 8.4.10, "Exclusion of Foreign Material from Plant Components and

Systems," and was a performance deficiency.

The finding was determined to be more than minor because it was associated with the

Barrier Integrity Cornerstone attribute of human performance and adversely affected the

associated cornerstone objective of providing reasonable assurance that physical design

barriers protect the public from radionuclide releases caused by accidents or events.

Specifically, due to the interference caused by the foreign material inside the 2SI-897B

valve, the valve would not have been able to perform its safety function to close during

the initiation of the post-LOCA sump-recirculation phase of safety injection.

The inspectors determined the finding could be evaluated in accordance with IMC 0609,

Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, Table 4a, containment barrier column, dated

January 10, 2008. The finding was determined to be of very low safety significance

(Green) because the issue did not represent a degradation of the radiological barrier

function provided for the control room, or auxiliary building, or spent fuel pool; represent

a degradation of the barrier function of the control room against smoke or a toxic

atmosphere; represent an actual open pathway in the physical integrity of reactor

containment (valves, airlocks, containment isolation system (logic and instrumentation)),

and heat removal components; nor involve an actual reduction in function of hydrogen

ignitors in the reactor containment. No cross-cutting aspect was identified because the

foreign material was determined to have been introduced into the system in the past and

was not considered indicative of current performance.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Specifically, procedure NP 8.4.10, required, in part, that

maintenance activities preclude the introduction of foreign material into the SI system.

Contrary to this, prior to October 17, 2009, the licensee failed to accomplish activities

affecting the quality of the SI system in accordance with the documented instructions

and procedures associated with the exclusion of foreign material from safety-related

plant equipment and systems, an activity affecting quality. Specifically, during a

Enclosure

19

previous work activity involving an open safety-related fluid system boundary, such as

the RWST, the licensee failed to adequately control foreign material in accordance with

procedure NP 8.4.10. Because this violation was of very low safety significance and

was entered into the licensees CAP as AR 011588112, "2SI897B Failed to Operate,"

this violation is being treated as an NCV, consistent with Section VI.A.1 of the

NRC Enforcement Policy (NCV 05000301/2009005-02).

In response to this issue, the licensee took prompt corrective actions to repair the valve

and perform an extent-of-condition review, including a boroscope inspection of the

upstream and downstream piping. Additionally, upon entering the issue into its CAP, the

licensee performed a causal evaluation to determine the most probable location through

which the foreign material entered and to develop appropriate corrective actions.

.2

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following issues:

AR 01161636; New Auxiliary Feedwater Line in Contact with Service Water Pipe;

AR 01160262; 1HX-I5C CFC Flow Out-of-Limit Low per TS-33;

AR 01158549; U2R20 Mode 3 UT [ultrasonic testing] Results - GL 08-01; and

AR 01159784; Spent Fuel Pool Pump Suction Isolation Valve Stem Contacting

Adjacent Pipe Insulation.

The inspectors selected this potential operability issue based on the risk significance of

the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability and system functionality were

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the TSs and FSAR to the licensee's

evaluations to determine whether the components or systems were operable or

functional. Where compensatory measures were required to maintain operability, the

inspectors determined whether the measures in place would function as intended and

were properly controlled. The inspectors determined, where appropriate, compliance

with bounding limitations associated with the evaluations. Additionally, the inspectors

also reviewed a sampling of corrective action documents to verify that the licensee was

identifying and correcting any deficiencies associated with operability evaluations.

Documents reviewed are listed in the Attachment to this report.

This operability inspection constituted four samples as defined in IP 71111.15-05.

b.

Findings

No findings of significance were identified.

Enclosure

20

1R18 Plant Modifications (71111.18)

.1

Temporary Plant Modifications

a.

Inspection Scope

The inspectors reviewed the following temporary modification:

modifications in Unit 2 turbine building to facilitate installation of new feedwater

heaters.

The inspectors compared the temporary configuration changes and associated

10 CFR 50.59 screening and evaluation information against the design basis, the FSAR,

and the TSs, as applicable, to verify that the modification did not affect the operability or

availability of the affected systems. The inspectors also compared the licensee's

information to operating experience information to ensure that lessons learned from

other utilities had been incorporated into the licensee's decision to implement the

temporary modification. The inspectors, as applicable, performed field verifications to

ensure that the modifications were installed as directed; the modifications operated as

expected; modification testing adequately demonstrated continued system operability,

availability, and reliability; and that operation of the modifications did not impact the

operability of any interfacing systems. Lastly, the inspectors discussed the temporary

modification with operations, engineering. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted one temporary modification sample as defined in

IP 71111.18-05.

b.

Findings

Failure to Update Safe Load Path Manual to Include Safety-Related Cable Locations

Introduction: A finding of very low safety significance and associated NCV of

10 CFR Part 50, Appendix B, Criterion III, "Design Control," was identified for the failure

to ensure that the safe load path (SLP) and rigging manual for the Unit 2 turbine building

crane (SLP-3), was updated as part of the major safety-related modification that added

the G-03 and G-04 EDGs in 1995 and 1996.

Description: On October 14, 2009, the licensee generated AR 1158472, which captured

an NRC-identified concern regarding the adequacy of SLP-3 with respect to the G-03

and G-04 modifications. Specifically, it was identified that SLP-3 allowed unrestricted

load lifts over the U2 turbine building truck-bay area based upon evaluations performed

in the early 1980s in response to NRC GL 81-07 "Control of Heavy Loads," and was not

updated to reflect changes to the design of the facility when the G-03 and G-04 EDGs

were installed and a modification added safety-related, risk-significant, cables under the

Unit 2 truck bay in 1995 and 1996. These cables included the 4160-volt AC output

cables from the train B EDGs (G-03 and G-04), and the 480-volt AC power cables to

the train A EDGs (G-01 and G-02) fuel oil transfer pumps. Due to the close proximity

of A and B train cables, a loss of both trains of emergency AC power could result if

the underground cables were disabled by a postulated dropped load of sufficient

Enclosure

21

magnitude, such as a drop of the spare low pressure turbine rotor from the 66-foot

elevation.

On September 30, 2009, the inspectors initially queried the licensee about upcoming

Unit 2 feedwater (FW) heater replacement activities, with heavy load lifts scheduled for

the Unit 2 truck bay during the fall 2009 RFO. Specifically, the inspectors inquired about

the underground cables and whether or not the licensee had accounted for them in the

preparations for the FW heater removals and installations with regard to potential load

drop effects. When the inspectors asked for the licensee's justification for why a load

drop analysis had not been performed, the licensee stated that it was unnecessary

because SLP-3 allowed for unrestricted load lifts in that area.

When the inspectors examined the basis for SLP-3, it was noted that the plan for that

area had remained essentially unchanged since its initial creation in the early 1980s,

before the installation of the G-03 and G-04 EDGs in 1995 and 1996. It became evident

to the inspectors that the SLP-3 had not been sufficiently revised to account for the

existence of the risk-significant cables under the Unit 2 truck bay.

As a result of these discussions, the licensee determined that a 2 inch-thick layer of steel

plates would be temporarily installed under the FW heater load lift area to provide

adequate protection for the cables in the event of a load drop.

Analysis: The inspectors determined that the failure to update the SLP-3 as a part of the

engineering change process when the diesel generator modification was implemented

was contrary to the requirements of 10 CFR Part 50, Appendix B, Criterion III,

"Design Control," and was a performance deficiency.

The finding was more than minor because it was associated with the Mitigating Systems

Cornerstone attribute of design control and adversely affected the associated

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core

damage). In accordance with NRC IMC 0609, Appendix A, "Significance Determination

of Reactor Inspection Findings for At-Power Situations," dated January 10, 2008, the

inspectors conducted a Phase 1 SDP screening and determined the finding to be of very

low safety significance (Green) because the finding was not a design or qualification

deficiency, did not represent a loss of system safety function or loss of a single train for

greater than its allowed technical specification time, and did not screen as potentially

risk-significant due to seismic, flooding, or severe weather initiating events.

This finding has a cross-cutting aspect in the area of problem identification and

resolution, CAP, because the staff did not take appropriate corrective actions to address

safety issues in a timely manner, commensurate with their safety significance.

Specifically, when AR 1122278 from February 2008 raised similar questions regarding

the adequacy of SLP-3, no revision to the SLP resulted, despite one being drafted at the

time. That AR was closed in April 2009 to no actions taken. Inspectors viewed that AR

as a missed opportunity for the site to resolve the SLP-3 issue (P.1(d)).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,

in part, that measures be established to assure that applicable regulatory requirements

and the design basis are correctly translated into specifications, drawings, procedures,

and instructions. Contrary to this, from initial in-service installation of the G-03 and G-04

Enclosure

22

EDGs, to the point when SLP-3 was corrected in October 2009, the licensee failed to

ensure that the design bases changes to the EDG system were correctly translated into

specifications, drawings, procedures, and instructions. Because this violation was of

very low safety significance and was entered into the licensees CAP, as AR 1158472,

this violation is being treated as an NCV, consistent with Section VI.A.1 of the

NRC Enforcement Policy (NCV 05000301/2009005-03).

The licensee's corrective actions addressed the immediate concern by installing

temporary steel plates over the affected area of the truck bay to provide adequate

protection for upcoming heavy load lifts. Additionally, the licensee revised SLP-3 to

require additional risk mitigation measures be taken prior to any future heavy load lifts in

that area.

.2

Permanent Plant Modifications

a.

Inspection Scope

The following engineering design packages were reviewed and selected aspects were

discussed with engineering personnel:

GSI 191 (Generic Safety Issue) modifications EC [Engineering Change] 13601 -

RCP [Reactor Coolant Pump] S/G, and RCS Loops Piping Insulation

Replacement - Unit 2, and EC 12601 - Additional Sump Strainer Modules -

Unit 2; and

EC 11542; Unit 2 Main Generator Circuit Breaker Addition.

These documents and related documentation were reviewed for adequacy of the

associated 10 CFR 50.59 safety evaluation screening, consideration of design

parameters, implementation of the modification, post-modification testing, and proper

update of relevant procedures, design, and licensing documents. The inspectors

observed ongoing and completed work activities to verify that installation was consistent

with the design control documents. The first sample was for the modification that

replaced the Unit 2 main generator circuit breaker, and the other sample was for

GSI-191 modifications in the Unit 2 containment that replaced insulation and added

additional sump strainer modules. Documents reviewed are listed in the Attachment to

this report.

Specifically, the inspectors conducted a walkdown of the strainer assemblies during the

fall 2009 RFO for Unit 2. The engineering design packages were associated with the

licensee's response to GL 2004-02, "Potential Impact of Debris Blockage on Emergency

Recirculation During Design Basis Accidents at Pressurized-Water Reactors."

The licensee's implementation of commitments documented in its initial responses to

GL 2004-02 was previously reviewed in accordance with temporary instruction

(TI) 2515/166, "Pressurized Water Reactor Containment Sump Blockage." The

closure of this TI in the summer 2008, documented in NRC Inspection Report (IR)

05000266/2008003; 05000301/2008003, indicated that the licensee had received

approval for an extension for GL 2004-02 corrective actions.

In July 2008, after the establishment of an industry head loss test protocol, the licensee

conducted additional testing using the revised test methodologies. During this testing,

the licensee determined that the original containment sump strainer modification of

Enclosure

23

11 strainer modules per train, which had already been installed, did not meet test

acceptance criteria. As a result, the licensee installed three additional strainers modules

per train, added debris interceptors, removed fibrous insulation in the fall 2008 RFO for

Unit 1, and planned similar modifications for the fall 2009 RFO for Unit 2. The purpose

of the modification was to obtain additional net positive suction head margin for the

residual heat removal pumps. However, prototypical testing of the debris interceptors in

January 2009 indicated that the efficiency of the debris interceptors was not as high as

required. In order to address this issue and recent concerns regarding the assumed

destruction zone of influence for fibrous insulation, the licensee planned to remove

additional fibrous insulation and revise the debris generation and transport analyses

accordingly. Specifically, the licensee developed an additional modification that reduced

the amount of fibrous insulation debris by replacing the existing insulation with metallic

reflective insulation on reactor coolant pumps bowl assemblies, portions of steam

generators, and portions of reactor coolant system loop piping.

The licensee requested and received NRC approval for an extension for GL 2004-02

corrective actions to June 30, 2010, for Unit 1, and June 20, 2011, for Unit 2. Since the

closure of TI 2515/166, the licensee has completed the following actions:

installation of an additional three strainer modules per train to increase the

overall surface area in Units 1 and 2;

installation of debris interceptors to reduce the quantity of suspended debris that

could be transported to the screen surface in Unit 1;

structural reinforcement of the strainer assemblies to accommodate an increased

differential pressure in Unit 2;

extension of the refueling cavity drain line away from the strainers in order to

prevent water from spilling on or near the strainers and potentially causing air

ingestion in Units 1 and 2; and

initiated the fibrous insulation reduction effort in Units 1 and 2.

The outstanding actions are:

complete the fibrous insulation reduction effort during the spring 2010 RFO for

Unit 1 and the spring 2011 RFO for Unit 2; and

update the licensing bases as required.

This inspection constituted two permanent plant modification samples as defined in

IP 71111.18-05.

b.

Findings

Potential Failure To Adequately Evaluate Seismic II/I Concerns For Units 1 And 2

B Containment Sump Strainers

Introduction: The inspectors identified an unresolved item (URI) regarding the B

containment sump strainers for Units 1 and 2. Specifically, the inspectors questioned

Enclosure

24

whether the ventilation ducts located above containment sump strainers were

adequately evaluated with respect to seismic II/I considerations.

Description: On October 27, 2009, the inspectors performed a walkdown of the

containment sump strainers of Unit 2 and noted a ventilation duct located above the

B containment sump strainer. The inspectors were concerned that during a seismic

event the structure could collapse and affect the strainers ability to fulfill its accident

mitigating function. Specifically, if the ventilation duct and its support structure

collapsed, the structural integrity of the sump strainer could be compromised or the

failed duct and support could block the strainers. The sump strainers are relied upon to

simultaneously maintain an adequate post-loss-of-coolant-accident suction source while

preventing debris from entering the emergency core cooling system.

The licensee's immediate documentation search on the seismic evaluation of the

ventilation duct was unsuccessful. The licensee initiated AR 01159937. The licensee

also determined that the same condition existed in Unit 1 and performed a prompt

operability determination for the Unit 1 B strainer.

The licensee later determined that the installation modification documentation for Unit 1,

Engineering Change (EC) 1602, indicated that the modification did not require analysis

of non-seismic components located over or adjacent to seismic components because

there was no evidence of a potential seismic II/I concern at the time the modification was

completed. Specifically, a seismic interaction walkdown was required in the installation

work plan prior to the installation of the strainers. The walkdown was completed by two

civil engineers who were Seismic Qualification Users Group (SQUG) qualified.

The licensee determined, through discussions with the engineers who performed the

walkdown, that the ventilation ducts were reviewed. Based on these facts, the licensee

concluded that: (1) the ventilation ducts were seismically evaluated; (2) the evaluation

determined that there are no seismic II/I concerns; and (3) that this is a documentation

issue. The same conclusions applied to Unit 2.

However, the inspectors were concerned with the use of SQUG methodology to

evaluate the seismic II/I interactions with respect to the duct ventilation and the strainer.

Specifically, the inspectors questioned whether this methodology could be applied to

ventilation ducts because this type of structure did not appear in the equipment classes

of the implementing procedure for SQUG. As a result of the inspectors' questions,

the licensee performed a prompt operability determination, in accordance with

EN-AA-203-1001 that determined the Unit 1 B sump strainer was operable. The

basis for this conclusion was documented in EC 14790. This EC performed a structural

analysis that concluded that the ventilation duct support structure would be able to

support loads induced by a seismic event. Again, this evaluation applied to Unit 2.

In addition, the inspectors noted that the FSAR, Appendix A5.6, stated that

"Modified, new, or replacement equipment classified as Seismic Class I may be

seismically designed and verified (after installation) for seismic adequacy using seismic

experience data in accordance with a methodology developed by the SQUG." It was not

clear whether this statement applied for all new modifications or to the replacement of

previously SQUG-qualified equipment with similar equipment.

The inspectors were also concerned with the level of documentation maintained by the

licensee for the walkdowns performed using the SQUG methodology. Specifically, the

Enclosure

25

inspectors noted that the documentation did not provide the necessary details to permit

independent auditing of the inferences or conclusions.

This issue is unresolved pending further NRC review of the licensing basis for the use of

SQUG methodology and determination of further NRC actions to resolve the issues

(URI 05000266/2009005-04; 05000301/2009005-04).

1R19 Post-Maintenance Testing (71111.19)

.1

Post-Maintenance Testing (PMT)

a.

Inspection Scope

The inspectors reviewed the following PMT activities to verify that procedures and test

activities were adequate to ensure system operability and functional capability:

auxiliary feedwater and containment spray systems post-weld testing;

TS-82 monthly EDG run PMT for annual maintenance and failed level switch in

sump tank;

RHR pump 2P-10B PMT after oil leak repair; and

Unit 2 polar crane PMT following cable replacement.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TSs, the FSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted four post-maintenance testing samples as defined in

IP 71111.19-05.

b.

Findings

No findings of significance were identified.

Enclosure

26

1R20 Outage Activities (71111.20)

.1

Refueling Outage Activities

a.

Inspection Scope

The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 2

RFO, conducted October 15 - December 5, 2009, to confirm that the licensee had

appropriately considered risk, industry experience, and previous site-specific problems in

developing and implementing a plan that assured maintenance of defense-in-depth.

During the RFO, the inspectors observed portions of the shutdown and cooldown

processes and monitored licensee controls over the outage activities listed below.

Documents reviewed are listed in the Attachment to this report.

Licensee configuration management, including maintenance of defense-in-depth

commensurate with the Outage Safety Plan for key safety functions and

compliance with the applicable TS when taking equipment out-of-service.

Implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing.

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error.

Controls over the status and configuration of electrical systems to ensure that

TS and Outage Safety Plan requirements were met, and controls over switchyard

activities.

Monitoring of decay heat removal processes, systems, and components.

Controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system.

Reactor water inventory controls, including flow paths, configurations, and

alternative means for inventory addition, and controls to prevent inventory loss.

Controls over activities that could affect reactivity.

Maintenance of secondary containment as required by TS.

Refueling activities, including fuel handling and activities to detect fuel assembly

leakage.

Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of containment to verify that debris had not been left which could block

emergency core cooling system suction strainers, and reactor physics testing.

Licensee identification and resolution of problems related to RFO activities.

This inspection constituted one refueling outage sample as defined in IP 71111.20-05.

b.

Findings

Momentary Loss of Unit 2 Reactor Vessel Level Indication in the Control Room

Introduction: A finding of very low safety significance and associated Green NCV of

10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," was

self-revealed when the licensee performed an Instrumentation and Control (I&C)

procedure that was inappropriate to the circumstances and caused the momentary loss

of all available channels of reactor vessel level indication in the control room.

Enclosure

27

Description: On October 19, 2009, operators were maintaining reactor vessel inventory

at 70 percent in preparation for head disassembly and placed the reduced inventory

reactor vessel level transmitters (LT), LT-447 and LT-447A, into service for level

indication. Subsequently, the operators authorized maintenance to perform

I&C procedure 2ICP 04.023-1, "Reactor Vessel Level Outage Calibration." The purpose

of the procedure was to calibrate reactor vessel wide and narrow range level

transmitters, 2LT-494, 2LT-495, 2LT-496, and 2LT-497.

During the performance of this procedure, following calibration of 2LT-494, the

technician valved in the transmitter. This allowed a flow path to exist between the

variable and common reference legs of all the reactor vessel level indicators, which

caused a perturbation on the level indication for 2LT-447 and 2LT-447A, and

subsequent momentary loss of reactor vessel level indication in the control room.

The operators took immediate action to suspend the performance of the I&C procedure

and sent an operator into containment to verify reactor vessel level via the local

standpipe level indicator (LI), LI-447B, and to ensure level indication was reestablished.

The I&C procedure contained instructions to notify the control operator that perturbations

on the reactor vessel level indicators 2LT-447 and 2LT-447A may occur and required

operators to verify reduced inventory conditions were not in effect. However, the

procedure did not contain cautions or prerequisite conditions for the given conditions of

being at 70 percent inventory and time-to-boil (TTB) of 17 minutes, essentially the same

TTB as a reduced inventory condition. No additional barriers were in place to prevent

the procedure from being performed at the same time as preparations for head

disassembly.

Analysis: A performance deficiency was identified when the licensee performed an

I&C procedure that was inappropriate for the circumstances of reactor vessel level at

70 percent and a TTB of 17 minutes; thereby, causing a loss of all available channels of

reactor vessel level indication in the control room. The finding was more than minor

because it is associated with the Mitigating Systems Cornerstone attribute of procedure

quality and adversely affected the associated cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

In accordance with NRC IMC 0609, Appendix G, "Shutdown Operations Significance

Determination Process," Attachment 1, Checklist 3, dated May 25, 2004, the inspectors

conducted a Phase 1 SDP screening and determined that the finding required a Phase 2

analysis since the finding increased the likelihood of a loss of RCS inventory based on

loss of reactor vessel level indication in the control room (Sections II(A)(2) II(B)(3) of

Checklist 3).

A Region III senior reactor analyst (SRA) performed the assessment using Appendix G,

Attachment 2, "Phase 2 Significance Determination Process Template for PWR During

Shutdown," dated February 28, 2005. The SRA determined this to be a precursor to an

initiating event (a loss of level control precursor - LOLC). The plant operating state

(POS) was determined to be "POS 1" (vessel head on and RCS closed). The initiating

event likelihood for LOLC using Table 1, "Initiating Event Likelihood (IELs) for LOLC

Precursors" was "1," since the time to RHR loss was greater than two hours and action

to recover RHR could be identified and performed within half of the time to RHR loss.

The SRA considered this to be an overly conservative value considering that there was

Enclosure

28

no actual loss of RCS inventory, only momentary loss of indication. To better estimate

the IEL, the SRA performed an analysis using the SPAR-H Human Reliability Analysis

Method, NUREG/CR-6883, September 2004.

For diagnosis of potential loss of level control, the analyst assumed available time to be

expansive. For action, the analyst assumed stress to be high. All other performance

shaping factors were assumed to be nominal. The resultant value of 3E-3 was assumed

as the initiating event likelihood.

Using Appendix G, Attachment 2, Worksheet 1, "SDP for a PWR Plant - Loss Level

Control in POS 1 (RCS Closed)," the SRA evaluated the remaining mitigating capability

credit to reflect equipment availability and the time available to complete tasks prior to

core damage. The most significant core damage sequences involved loss of steam

generator cooling and failure of RCS injection and bleed before core damage. The

combined sequences had a risk significance of about 3E-8. Therefore, the SRA

determined that this issue is best characterized as a finding of very low safety

significance (Green).

The finding had a cross-cutting aspect in the area of human performance, work control

aspect, in that the licensee did not appropriately coordinate work activities for the

existing plant conditions to ensure the operational impact on reactor vessel level

indication while at a water level near reduced inventory (H.3(b)).

Enforcement: Title 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and

Drawings," requires, in part, that activities affecting quality be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances and be

accomplished in accordance with these instructions, procedures or drawings. Contrary

to this, the licensee performed an I&C procedure that was inappropriate to the

circumstances. Specifically, I&C procedure 2ICP 04.023-1, disabled all control room

reactor vessel level indication while the reactor coolant system was at 70 percent reactor

vessel level. As a result, the indication of reactor water level in the reduced inventory

range was momentarily lost in the control room, which was not appropriate for the

current plant condition. Because this violation was of very low safety significance and it

was entered into the licensee's CAP (AR 01158914), this violation is being treated as an

NCV consistent with section VI.A.1. of the NRC Enforcement Policy

(NCV 05000301/2009005-05).

The licensee took immediate action to suspend the performance of the I&C procedure

and sent an operator into containment to verify reactor vessel level via the local

standpipe level indicator (LI-447B) to ensure level indication was reestablished.

Additionally, the licensee has applied work planning logic to this activity to ensure the

reactor is defueled prior to beginning the calibration and is evaluating necessary

revisions to the I&C procedure.

Enclosure

29

1R22 Surveillance Testing (71111.22)

.1

Surveillance Testing

a.

Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

Unit 2 ORT 3A/B EDG loss of offsite power loss of coolant accident routine test;

OSHA [Occupational Safety and Health Administration] polar crane inspection;

and

Unit 2 turbine-driven AFW pump and valve inservice test.

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

did preconditioning occur;

were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as-left setpoints were within required ranges; and the calibration frequency were

in accordance with TSs, the USAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of ASME Code Section XI, and reference

values were consistent with the system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

Enclosure

30

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two routine surveillance testing samples and one inservice

testing sample as defined in IP 71111.22, Sections -02 and -05.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System (ANS) Evaluation (71114.02)

.1

ANS Evaluation

a.

Inspection Scope

The inspectors reviewed documents and conducted discussions with Emergency

Preparedness (EP) staff and management regarding the operation, maintenance, and

periodic testing of the ANS in the Point Beach Plant's plume pathway Emergency

Planning Zone. The inspectors reviewed monthly trend reports and the daily and

monthly operability records from October 2007 through November 2009. Information

gathered during document reviews and interviews was used to determine whether the

ANS equipment was maintained and tested in accordance with Emergency Plan

commitments and procedures. Documents reviewed are listed in the Attachment to this

report.

This alert and notification system inspection constituted one sample as defined in

IP 71114.02-05.

b.

Findings

No findings of significance were identified.

1EP3 Emergency Response Organization (ERO) Augmentation Testing (71114.03)

.1

ERO Augmentation Testing

a.

Inspection Scope

The inspectors reviewed and discussed with plant EP management and staff the

emergency plan commitments and procedures that addressed the primary and alternate

methods of initiating an ERO activation to augment the on-shift ERO as well as the

provisions for maintaining the station's ERO qualification and team lists. The inspectors

reviewed reports and a sample of CAP records of unannounced off-hour augmentation

tests and pager test, which were conducted between March 2008 and September 2009,

Enclosure

31

to determine the adequacy of the drill critiques and associated corrective actions. The

inspectors also reviewed a sample of the EP training records of approximately

37 ERO personnel, who were assigned to key and support positions, to determine the

status of their training as it related to their assigned ERO positions. Documents

reviewed are listed in the Attachment to this report.

This emergency response organization augmentation testing inspection constituted one

sample as defined in IP 71114.03-05.

b.

Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

.1

Emergency Action Level and Emergency Plan Changes

a.

Inspection Scope

Since the last NRC inspection of this program area, emergency action level and

Emergency Plan revisions were implemented based on the licensees determination, in

accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in

effectiveness of the Plan, and that the revised Plan as changed continues to meet the

requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. Revisions to the

emergency action levels and emergency plan reviewed by the inspectors included:

1) EP 2.0, Revision 46; 2) EP 6.0, Revisions 51 and 52; 3) Appendix M, Revision 2; and

4) EPIP 1.2.1, Revision 3. The inspectors conducted a sampling review of the

Emergency Plan changes and a review of the Emergency Action Level changes to

evaluate for potential decreases in effectiveness of the Plan. However, this review does

not constitute formal NRC approval of the changes. Therefore, these changes remain

subject to future NRC inspection in their entirety.

This emergency action level and emergency plan changes inspection constituted one

sample as defined in IP 71114.04-05.

b.

Findings

No findings of significance were identified.

1EP5 Correction of EP Weaknesses and Deficiencies (71114.05)

.1

Correction of EP Weaknesses and Deficiencies

a.

Inspection Scope

The inspectors reviewed a sample of Nuclear Oversight 2008 and 2009 audits of the

Point Beach EP program to determine that the independent assessments met the

requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports and

samples of CAP records associated with the 2008 biennial exercise, as well as various

EP drills conducted in 2007, 2008, and 2009, in order to determine whether the licensee

fulfilled drill commitments and to evaluate the licensee's efforts to identify and resolve

Enclosure

32

identified issues. The inspectors reviewed a sample of EP items and corrective actions

related to the facility's EP program and activities to determine whether corrective actions

were completed in accordance with the site's CAP. Documents reviewed are listed in

the Attachment to this report.

This correction of emergency preparedness weaknesses and deficiencies inspection

constituted one sample as defined in IP 71114.05-05.

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1

Review of Licensee Performance Indicators (PIs) for the Occupational Exposure

Cornerstone

a.

Inspection Scope

The inspectors reviewed the licensee's Occupational Exposure Control Cornerstone PI

to determine whether the conditions resulting in any PI occurrences had been evaluated

and whether identified problems had been entered into the licensee's CAP for resolution.

This inspection constituted one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.2

Plant Walkdowns and Radiation Work Permit (RWP) Reviews

a.

Inspection Scope

The inspectors reviewed licensee controls and surveys in the following radiologically

significant work areas within radiation areas, high radiation areas, and airborne

radioactivity areas in the plant to determine if radiological controls including surveys,

postings, and barricades were acceptable:

Auxiliary Building;

Containment Building;

Spent Fuel Pool.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors reviewed the RWPs and work packages used to access these areas and

other high radiation work areas. The inspectors assessed the work control instructions

and control barriers specified by the licensee. Electronic dosimeter alarm setpoints for

Enclosure

33

both integrated dose and dose rate were evaluated for conformity with survey indications

and plant policy. The inspectors interviewed workers to verify that they were aware of

the actions required if their electronic dosimeters noticeably malfunctioned or alarmed.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors walked down and surveyed (using an NRC survey meter) these areas to

verify that the prescribed RWP, procedure, and engineering controls were in place; that

licensee surveys and postings were complete and accurate; and that air samplers were

properly located.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors reviewed RWPs for airborne radioactivity areas to verify barrier integrity

and engineering controls performance (e.g., high-efficiency particulate air ventilation

system operation) and to determine if there was a potential for individual worker internal

exposures in excess of 50 millirem committed effective dose equivalent (EDE). There

were no airborne radioactivity work areas during the inspection period.

Work areas having a history of, or the potential for, airborne transuranics were evaluated

to verify that the licensee had considered the potential for transuranic isotopes and had

provided appropriate worker protection.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors assessed the adequacy of the licensee's internal dose assessment

process for internal exposures in excess of 50 millirem committed EDE. There were no

internal exposures greater than 50 millirem committed EDE.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors also reviewed the licensee's physical and programmatic controls for

highly activated and/or contaminated materials (non-fuel) stored within the spent fuel

pool or other storage pools.

This inspection constituted one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.3

Problem Identification and Resolution

a.

Inspection Scope

The inspectors reviewed a sample of the licensee's self-assessments, audits, Licensee

Event Reports (LERs), and Special Reports related to the access control program to

verify that identified problems were entered into the CAP for resolution.

This inspection constituted one sample as defined in IP 71121.01-5.

Enclosure

34

The inspectors reviewed corrective action reports related to access controls and any

high radiation area radiological incidents (issues that did not count as PI occurrences

identified by the licensee in high radiation areas less than 1R/hr). Staff members were

interviewed and corrective action documents were reviewed to verify that follow-up

activities were being conducted in an effective and timely manner commensurate with

their importance to safety and risk based on the following:

initial problem identification, characterization, and tracking;

disposition of operability/reportability issues;

evaluation of safety significance/risk and priority for resolution;

identification of repetitive problems;

identification of contributing causes;

identification and implementation of effective corrective actions;

resolution of NCVs tracked in the corrective action system; and

implementation/consideration of risk significant operational experience feedback.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors evaluated the licensee's process for problem identification,

characterization, and prioritization and verified that problems were entered into the CAP

and resolved. For repetitive deficiencies and/or significant individual deficiencies in

problem identification and resolution, the inspectors verified that the licensee's

self-assessment activities were capable of identifying and addressing these deficiencies.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors reviewed licensee documentation packages for all PI events occurring

since the last inspection to determine if any of these PI events involved dose rates in

excess of 25 R/hr at 30 centimeters or in excess of 500 R/hr at 1 meter. Barriers were

evaluated for failure and to determine if there were any barriers left to prevent personnel

access. Unintended exposures exceeding 100 millirem total EDE (or 5 rem shallow

dose equivalent or 1.5 rem lens dose equivalent) were evaluated to determine if there

were any regulatory overexposures or if there was a substantial potential for an

overexposure.

This inspection constituted one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.4

Job-In-Progress Reviews

a.

Inspection Scope

The inspectors observed the following three jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers:

Enclosure

35

insulation activities;

reactor coolant pump activities; and

core barrel movement activities.

The inspectors reviewed radiological job requirements for these activities, including

RWP requirements and work procedure requirements, and attended

As-Low-As-Is-Reasonably-Achievable (ALARA) job briefings.

This inspection constituted one sample as defined in IP 71121.01-5.

Job performance was observed with respect to the radiological control requirements to

assess whether radiological conditions in the work area were adequately communicated

to workers through pre-job briefings and postings. The inspectors evaluated the

adequacy of radiological controls, including required radiation, contamination, and

airborne surveys for system breaches; radiation protection job coverage, including any

applicable audio and visual surveillance for remote job coverage; and contamination

controls.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors reviewed radiological work in high radiation work areas having significant

dose rate gradients to evaluate whether the licensee adequately monitored exposure to

personnel and to assess the adequacy of licensee controls. These work areas involved

areas where the dose rate gradients were severe, thereby increasing the necessity of

providing multiple dosimeters or enhanced job controls.

This inspection constituted one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.5

High Risk Significant, High Dose Rate, High Radiation Area, and Very High Radiation

Area Controls

a.

Inspection Scope

The inspectors held discussions with the Radiation Protection Manager concerning high

dose rate, high radiation area, and very high radiation area controls and procedures,

including procedural changes that had occurred since the last inspection, in order to

assess whether any procedure modifications substantially reduced the effectiveness and

level of worker protection.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors discussed with radiation protection supervisors the controls that were in

place for special areas of the plant that had the potential to become very high radiation

areas during certain plant operations. The inspectors assessed if plant operations

required communication beforehand with the radiation protection group, so as to allow

corresponding timely actions to properly post and control the radiation hazards.

Enclosure

36

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors conducted plant walkdowns to assess the posting and locking of

entrances to high dose rate, high radiation areas, and very high radiation areas.

This inspection constituted one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.6

Radiation Worker Performance

a.

Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation safety work requirements. The inspectors

evaluated whether workers were aware of any significant radiological conditions in their

workplace, of the RWP controls and limits in place, and of the level of radiological

hazards present. The inspectors also observed worker performance to determine if

workers accounted for these radiological hazards.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors reviewed radiological problem reports for which the cause of the event

was due to radiation worker errors to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. Problems or

issues with planned or completed corrective actions were discussed with the Radiation

Protection Manager.

This inspection constituted one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.7

Radiation Protection Technician Proficiency

a.

Inspection Scope

During job performance observations, the inspectors evaluated radiation protection

technician performance with respect to radiation safety work requirements. The

inspectors evaluated whether technicians were aware of the radiological conditions in

their workplace, the RWP controls and limits in place, and if their performance was

consistent with their training and qualifications with respect to the radiological hazards

and work activities.

This inspection constituted one sample as defined in IP 71121.01-5.

The inspectors reviewed radiological problem reports for which the cause of the event

was radiation protection technician error to determine if there was an observable pattern

Enclosure

37

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems.

This inspection constituted one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

.1

Radiological Work Planning

a.

Inspection Scope

The inspectors compared the results achieved (including dose rate reductions and

person-rem used) with the intended dose established in the licensee's ALARA planning

for GSI-191 insulation removal activities. Reasons for inconsistencies between intended

and actual work activity doses were reviewed.

This inspection constituted one required sample as defined in IP 71121.02-5.

b.

Findings

No findings of significance were identified.

.2

Verification of Dose Estimates and Exposure Tracking Systems

a.

Inspection Scope

The licensee's process for adjusting exposure estimates or re-planning work (when

unexpected changes in scope, emergent work, or higher than anticipated radiation levels

were encountered) was evaluated. This included determining whether adjustments to

estimated exposure (intended dose) were based on sound radiation protection and

ALARA principles or whether they resulted from failures to adequately plan or to control

the work. The frequency of these adjustments was reviewed to evaluate the adequacy

of the original ALARA planning process.

This inspection constituted one required sample as defined in IP 71121.02-5.

b.

Findings

No findings of significance were identified.

.3

Problem Identification and Resolutions

a.

Inspection Scope

The inspectors reviewed the licensee's self-assessments, audits, and Special Reports

related to the ALARA program since the last inspection to determine if the licensee's

overall audit program's scope and frequency for all applicable areas under the

Occupational Radiation Safety Cornerstone met the requirements of 10 CFR 20.1101(c).

Enclosure

38

This inspection constituted one required sample as defined in IP 71121.02-5.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, and Occupational Radiation Safety

4OA1 PI Verification (71151)

.1

Mitigating Systems Performance Index (MSPI) - Heat Removal System

a.

Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI for

Unit 1 and Unit 2 for the third quarter 2008 through the second quarter of 2009.

To determine the accuracy of this PI data, definitions and guidance contained in the

Nuclear Energy Initiative (NEI) Document 99-02, "Regulatory Assessment Performance

Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's

operator narrative logs, corrective action reports, event reports, MSPI derivation reports,

and NRC integrated IRs for October 2008 through June 2009 to validate the accuracy of

the submittals. The inspectors reviewed the MSPI component risk coefficient to

determine if it had changed by more than 25 percent in value since the previous

inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensee's CAP database to determine if any problems

had been identified with the PI data collected or transmitted for this indicator.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI heat removal system samples as defined in

IP 71151-05.

b.

Findings

No findings of significance were identified.

.2

MSPI - RHR System

a.

Inspection Scope

The inspectors sampled licensee submittals for the MSPI Index - RHR System PI Unit 1

and Unit 2 for the third quarter 2008 through the second quarter of 2009. To determine

the accuracy of the PI data, definitions and guidance contained in NEI 99-02, Revision 5,

were used. The inspectors reviewed the licensee's operator narrative logs, issue

reports, MSPI derivation reports, event reports, and NRC Integrated IRs for October

2008 through June 2009, to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensee's

Enclosure

39

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted two MSPI RHR system sample as defined in IP 71151-05.

b.

Findings

No findings of significance were identified.

.3

Drill/Exercise Performance

a.

Inspection Scope

The inspectors sampled licensee submittals for the Drill/Exercise PI for the fourth quarter

2008 through third quarter 2009. To determine the accuracy of the PI data, definitions and

guidance contained in NEI 99-02, Revision 5, were used. The inspectors reviewed the

licensee's records associated with the PI to verify that the licensee accurately reported the

PI in accordance with relevant procedures and the NEI guidance. Specifically, the

inspectors reviewed licensee records and processes including procedural guidance on

assessing opportunities for the PI, and assessments of PI opportunities during

pre-designated control room simulator training sessions, performance during the 2008

biennial exercise, and performance during other drills. Documents reviewed are listed in

the Attachment to this report.

This inspection constitutes one drill/exercise performance sample as defined in

IP 71151-05.

b.

Findings

No findings of significance were identified.

.4

ERO Drill Participation

a.

Inspection Scope

The inspectors sampled licensee submittals for the ERO Drill Participation PI for the

fourth quarter 2008 through third quarter 2009. To determine the accuracy of the PI data,

definitions and guidance contained in NEI 99-02, Revision 5, were used. The inspectors

reviewed the licensee's records associated with the PI to verify that the licensee

accurately reported the indicator in accordance with relevant procedures and the

NEI guidance. Specifically, the inspectors reviewed licensee records and processes

including procedural guidance on assessing opportunities for the PI; performance during

the 2008 biennial exercise and other drills; and revisions of the roster of personnel

assigned to key emergency response organization positions. Documents reviewed are

listed in the Attachment to this report.

This inspection constitutes one ERO drill participation sample as defined in IP 71151-05.

Enclosure

40

b.

Findings

No findings of significance were identified.

.5

Alert and Notification System

a.

Inspection Scope

The inspectors sampled licensee submittals for the ANS PI for the fourth quarter 2008

through third quarter 2009. To determine the accuracy of the PI data, definitions and

guidance contained in NEI 99-02, Revision 5, were used. The inspectors reviewed the

licensee's records associated with the PI to verify that the licensee accurately reported the

indicator in accordance with relevant procedures and the NEI guidance. Specifically, the

inspectors reviewed licensee records and processes including procedural guidance on

assessing opportunities for the PI and results of periodic ANS operability tests.

Documents reviewed are listed in the Attachment to this report.

This inspection constitutes one ANS sample as defined in IP 71151-05.

b.

Findings

No findings of significance were identified.

.6

Occupational Exposure Control Effectiveness

a.

Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences PI for the third quarter 2008 through the third quarter 2009. To determine

the accuracy of the PI data, definitions and guidance contained in NEI 99-02,

"Regulatory Assessment Performance Indicator Guideline," Revision 6 (issued

October 2009), were used. The inspectors reviewed the licensee's assessment of the

PI for occupational radiation safety to determine if indicator related data was adequately

assessed and reported. To assess the adequacy of the licensee's PI data collection and

analyses, the inspectors discussed with radiation protection staff the scope and breadth

of its data review and the results of those reviews. The inspectors independently

reviewed electronic dosimetry dose rate and accumulated dose alarm and dose reports

and the dose assignments for any intakes that occurred during the time period reviewed

to determine if there were potentially unrecognized occurrences. The inspectors also

conducted walkdowns of locked high and very high radiation area entrances to

determine the adequacy of the controls in place for these areas. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one occupational radiological occurrences sample as defined

in IP 71151-05.

b.

Findings

No findings of significance were identified.

Enclosure

41

.7

Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent

Occurrences

a.

Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent TS/Offsite

Dose Calculation Manual Radiological Effluent Occurrences PI for the third quarter 2008

through the third quarter 2009. The inspectors used PI definitions and guidance

contained in NEI 99-02, Revision 6, to determine the accuracy of the PI data.

The inspectors reviewed the licensee's issue report database and selected individual

reports generated since this indicator was last reviewed to identify any potential

occurrences such as unmonitored, uncontrolled, or improperly calculated effluent

releases that may have impacted offsite dose. The inspectors reviewed gaseous

effluent summary data and the results of associated offsite dose calculations for selected

dates between the third quarter 2008 and the third quarter 2009 to determine if indicator

results were accurately reported. The inspectors also reviewed the licensee's methods

for quantifying gaseous and liquid effluents and determining effluent dose. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one radiological effluent technical specification/offsite dose

calculation manual radiological effluent occurrences sample as defined in IP 71151-05.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Review of Items Entered into the CAP

a.

Inspection Scope

As part of the various baseline IPs discussed in previous sections of this report, the

inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that they were being entered into the licensee's CAP at an

appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensee's CAP as a result of the inspectors' observations

are included in the attached List of Documents Reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

Enclosure

42

b.

Findings

No findings of significance were identified.

.2

Daily CAP Reviews

a.

Inspection Scope

To assist with the identification of repetitive equipment failures and specific human

performance issues for follow-up, the inspectors performed a daily screening of items

entered into the licensee's CAP. This review was accomplished through inspection of

the station's daily condition report packages.

These reviews were performed by procedure as part of the inspectors' daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b.

Findings

No findings of significance were identified.

.3

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensee's CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors' review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors'

review nominally considered the six-month period of July through December 2009,

although some examples extended beyond those dates where the scope of the trend

warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self-assessment reports, and Maintenance Rule evaluations. The inspectors

compared and contrasted their results with the results contained in the licensee's

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensee's trending reports were reviewed for adequacy.

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b.

Findings

No findings of significance were identified.

Enclosure

43

4OA5 Other Activities

.1

(Closed) URI 05000266/2009004-01; 05000301/2009004-01, Failure to Control

Radioactive Material Within the Radiologically Controlled Area Resulting in Unnecessary

Dose to Worker

a.

Inspection Scope

The inspectors reviewed additional information, including the licensee's dose

assessment, for an incident on May 21, 2009, that involved a contract worker who

received unnecessary radiation exposure while performing inspections of the licensee's

electrical transformers. The inspection was completed through in-office review of

documents generated by the licensee. The review included discussions with various

members of the licensee's staff, both in person and by teleconference. A dose

assessment completed by the licensee's consultant was reviewed and independently

validated by NRC staff. Documents reviewed are listed in the Attachment to this report.

This URI is closed.

b.

Findings

Introduction: A self-revealed finding of very low safety-significance (Green) and an

associated NCV of 10 CFR 20.1101(b) was identified for the failure to adequately control

radioactive material and prevent its inadvertent migration outside the RCA, as required

by licensee procedure.

Description: On May 21, 2009, a contract worker alarmed the security gatehouse portal

radiation monitors while attempting to exit the protected area following completion of

transformer inspections. The transformers are located outside the RCA but within the

protected area. Investigation by the licensee disclosed that the worker picked-up debris

(pieces of unmarked tape wadded-together to the size of a billiard ball) found lying near

one of the transformers, placed the debris in the front trouser pocket, and approximately

two hours later, after completing assigned work duties, alarmed the radiation monitors

upon attempted egress from the protected area. The ball of tape was subsequently

identified by the licensee to be radioactively contaminated, primarily with cobalt-60.

The licensee's radiation measurements of the wadded tape ball using portable survey

instruments identified contact gamma and beta dose rates of about 6 mrem/hour and

500 mrad/hour, respectively. Low levels of contamination were also identified on the

workers clothing, some personal items, and left hand. No contamination or other

contaminated debris was identified during follow-up surveys in/near the transformers.

The licensee performed an apparent cause evaluation (ACE) that determined the tape

was likely used to cover the ends of piping or contaminated hoses because one of the

pieces of tape had a two-inch diameter circular marking. During RFOs, the yard area

outside the facade access into the containment building was the transfer point for

materials/equipment into and out of the containment building. The containment building

equipment hatch was sometimes opened to the environment to facilitate movement of

equipment and supplies. The licensee surmised that since outage equipment/material

was transferred from the containment building at night and during windy conditions and

at times when portions of the outdoor RCA barrier fence was removed, the material

could have escaped the licensee's control without notice and blown into the transformer

area.

Enclosure

44

The contract worker frequented the site on an approximate monthly basis or less,

spending a few hours to inspect and perform minor maintenance on the licensee's main

power transformers. The individual had not entered an RCA while onsite that day, the

work was not governed by a RWP, and the individual was not provided dosimetry. The

worker's assigned duties did not involve exposure to radiation and the individual should

not have come into contact with any radioactive material. The individual completed the

licensee's Plant Access Training required for unescorted access into the protected area

but not Radiation Worker Training required for access into RCAs. The licensee had

classified the worker as a member of the public, as provided in its Plant Access Training,

because the individual had no need to enter RCAs and the worker's dose was expected

to be well within the public dose limits of 10 CFR 20.1301. Consequently, the NRC

concluded that the dose received by the contractor from exposure to the contaminated

tape was deemed to be "public dose" as defined in 10 CFR 20.1003.

A dose evaluation completed by the licensee's consultant determined that the EDE to

the worker's thigh from exposure to the contaminated ball of tape was approximately

one mrem. The evaluation was independently reviewed by NRC staff and found to be

technically adequate and consistent with guidance provided in NRC Regulatory Issue

Summary 2003-04, "Use of Effective Dose Equivalent in Place of the Deep Dose

Equivalent in Dose Assessments." The licensee's corrective action called for expanded

radiation protection staff oversight during movement of material in/out of the containment

building during outages and for any movement of radioactively contaminated materials in

outdoor areas. Also, a radiation protection procedure was revised to require a

post-outage walkdown of outdoor RCA boundaries to ensure no material escaped.

Additionally, the licensee planned to construct an enclosure so that storage/transfer of

contaminated materials could be performed indoors.

Analysis: The inspectors determined that the failure to adequately control radioactive

material and prevent its migration outside the RCA was a performance deficiency.

The inspectors concluded that the cause of the performance deficiency was reasonably

within the licensee's ability to foresee and correct and should have been prevented.

The finding was not subject to traditional enforcement since the incident did not have a

significant or potentially significant safety consequence, did not impact the NRC's ability

to perform its regulatory function, and was not willful.

In accordance with IMC 0612, the inspectors determined that the finding was more than

minor because it impacted the program and process attribute of the Public Radiation

Safety Cornerstone and adversely affected the associated cornerstone objective of

ensuring adequate protection of public health and safety from exposure to radiation.

Specifically, contaminated material with measured dose rates distinguishable from

background escaped the licensee's control outside the RCA and resulted in unnecessary

radiation exposure to a member of the public that was approximately one percent of the

public dose limit. The finding was assessed using the Public Radiation Safety-

Significance Determination Process and determined to be of very low safety significance

because: (1) it involved a radioactive material control problem that was contrary to

NRC requirements and the licensee's procedure; and (2) the dose impact to a member

of the public (the contract worker) was less than 5 mrem total EDE.

The licensee conducted a "why staircase" analysis as part of its ACE that focused on

why contaminated equipment was transferred/stored in outdoor areas (a contributor to

Enclosure

45

the problem) instead of why material control was compromised in this instance

(the fundamental cause). Given that the licensee elected to transfer equipment outdoors

during potentially unfavorable environmental conditions without adequate controls in

place, the cause of the radioactive material control problem was determined to involve a

cross-cutting component in the human performance area for inadequate work control.

Specifically, the licensee did not plan/coordinate work activities consistent with safety in

that job site conditions, including environmental conditions (high winds, night time work,

etc.), impacted human performance and consequently radiological safety during

movement of contaminated material and equipment (H.3.(a)).

Enforcement: Title 10 CFR 20.1101(b) requires that each licensee use to the extent

practical procedures based on sound radiation protection principles to achieve

occupational and public doses as low as is reasonably achievable. Licensee procedure

NP 4.2.25, Revision 14, "Release of Material, Equipment and Personal Items From

Radiologically Controlled Areas," implements 10 CFR 20.1101(b) and was established to

ensure that licensed material is controlled and that dose to the public is minimized.

Sections 2.1, 2.4, and 4.1 of the procedure require that radioactive material remain in

RCAs, and that contaminated items be monitored by qualified radiation protection

personnel to determine they are free from detectable radioactive contamination prior to

release. Contrary to these requirements, on May 21, 2009, radioactively contaminated

debris escaped the licensee's control, migrated outside the RCA, and was picked-up by

an individual resulting in unnecessary radiation exposure. Since the failure to control

radioactive material was of very low safety significance, corrective actions were

proposed as described above, and the issue was entered into the licensee's CAP as

AR 01150045, the violation is being treated as an NCV consistent with Section VI.A of

the NRC Enforcement Policy (NCV 05000266/2009005-06; 05000301/2009005-06).

.2

(Closed) NRC TI 2515/175, "Emergency Response Organization, Drill/Exercise

Performance Indicator, Program Review"

The inspectors performed TI 2515/175, ensured the completeness of the TI's

Attachment 1, and then forwarded the data to NRC Headquarters.

.3

(Open) NRC TI 2515/177, "Managing Gas Accumulation in Emergency Core Cooling,

Decay Heat Removal and Containment Spray Systems (NRC Generic Letter 2008-01)"

a.

Inspection Scope and Documentation

On October 27, 2009, the inspectors conducted a walkdown of normally inaccessible

portion of piping of the RHR system in sufficient detail to reasonably assure the

acceptability of the licensee's walkdowns (TI 2515/177, Section 04.02.d). The inspectors

also verified that the information obtained during the licensee's walkdown was consistent

with the items identified during the inspectors independent walkdown (TI 2515/177,

Section 04.02.c.3).

In addition, the inspectors verified that the licensee had isometric drawings that

described the RHR system configurations. Specifically, the inspectors verified the

following, related to the isometric drawings:

high point vents were identified;

high points that do not have vents were acceptably recognizable;

Enclosure

46

other areas where gas can accumulate and potentially impact subject system

operability, such as at orifices in horizontal pipes, isolated branch lines, heat

exchangers, improperly sloped piping, and under closed valves, were acceptably

described in the drawings or in referenced documentation;

horizontal pipe centerline elevation deviations and pipe slopes in nominally

horizontal lines that exceed specified criteria were identified;

all pipes and fittings were clearly shown; and

the drawings were up-to-date with respect to recent hardware changes and that

any discrepancies between as-built configurations and the drawings were

documented and entered into the CAP for resolution.

The inspectors noted that the isometric drawings were not accurate with respect to small

bore piping (TI 2515/177, Section 04.02.a). Specifically, the inspectors found two vent

valves and one small relief valve that were not shown in the isometric drawings.

Subsequently, the inspectors were informed by the licensee that the drawings were

developed to record dimensions and configurations necessary to perform pipe stress

analyses and that the scope of that effort excluded piping with a diameter less than

2.5 inches. Although these specific examples did not present an adverse impact to plant

safety at the time of the inspection, the inspectors questioned if the level of detail of the

isometric drawings was appropriate with regard to the Gas Accumulation Management

Program. The licensee captured the issue in its CAP as AR 01159839.

In addition, the inspectors verified that Piping and Instrumentation Diagrams (P&IDs)

accurately described the subject systems, that they were up-to-date with respect to

recent hardware changes, and any discrepancies between as-built configurations, the

isometric drawings, and the P&IDs were documented and entered into the CAP for

resolution (TI 2515/177, Section 04.02.b).

Documents reviewed are listed in the Attachment to this report.

This inspection effort counts towards the completion of TI 2515/177, which will be closed

in a later IR.

b.

Findings

No findings of significance were identified.

.4

Confirmatory Order EA-06-178 Actions (92702)

a.

Inspection Scope

In a letter dated January 3, 2007, (ADAMS Accession Number ML063630336),

the NRC issued a Confirmatory Order to the licensee as part of a settlement agreement

through the NRC's Alternative Dispute Resolution (ADR) program. The NRC

investigated an alleged violation of 10 CFR 50.7, "Employee Protection," to determine

whether a senior reactor operator was the subject of retaliation for raising a nuclear

safety concern in the licensees CAP. This issue was resolved through the

NRCs ADR program and was being tracked as Apparent Violation (AV)05000266/2006013-05; 05000301/2006013-05 pending continuing NRC review and

inspection of the licensees completion of the items specified in the Confirmatory Order.

Enclosure

47

The Order had been issued to the Nuclear Management Company (NMC), the previous

operator of the Point Beach plant.

From December 14 through 18, 2009, the inspectors utilized IP 92702, "Followup On

Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action

Letters, Confirmatory Orders, And Alternative Dispute Resolution Confirmatory Orders,"

to assess the licensees completion of the items contained in the Order. The inspectors

interviewed site personnel, observed training conducted in response to the Confirmatory

Order, performed document reviews, and reviewed some of the applicable corrective

actions the licensee had taken in response to the Confirmatory Order. An Office of

Enforcement Specialist assisted the inspectors.

In addition, the inspectors also assessed the results of the licensees independent

assessment of the corrective actions taken in response to the licensees 2004, 2006,

and 2008 culture surveys. This independent assessment was requested by the

NRC Region III Office in the March 4, 2009, Annual Assessment Letter.

The modifications to the facility license as a result of the Confirmatory Order included the

following items, in part:

1. By no later than nine (9) months after the issuance of this Confirmatory Order, the

Nuclear Management Company (NMC) agrees to review, revise, and communicate

to NMC employees and managers its policy relating to the writing of CAP reports,

and provide training to NMC employees and managers to clarify managements

expectation regarding the use of the program with the goal to ensure employees are

not discouraged, or otherwise retaliated or perceived to be retaliated against, for

using the CAP.

2. By no later than June 30, 2007, NMC agrees to communicate its safety culture policy

(including safety-conscious work environment (SCWE)) to NMC employees,

providing employees with the opportunity to ask questions in a live forum.

3. By no later than nine (9) months after the issuance of this Confirmatory Order,

NMC agrees to train its employees holding supervisory positions and higher who

have not had formal training on SCWE principles within the previous two years of the

Confirmatory Order. NMC agrees to use a qualified training instructor (internal or

external) for such training. NMC shall review and enhance, if necessary, its

refresher SCWE training consistent with NMCs refresher training program and

provide such refresher training to its employees. New employees holding

supervisory positions and higher shall be trained on SCWE principles within nine (9)

months of their hire dates unless within the previous two years of their hire dates,

they've had the same or equivalent SCWE training.

4. By no later than March 30, 2007, NMC shall develop action plans to address

significant issues identified as needing management attention in the NMC 2004 and

2006 Comprehensive Cultural Assessments at the Point Beach Nuclear Plant

(PBNP); to conduct focus group interviews with Priority 1 & 2 organizations to

understand the cause of the survey results; and to review and, as appropriate, reflect

nuclear industry best practices in its conduct of focus groups and action plans to

address the issues at PBNP. As part of the development of the action plans,

NMC shall also assess and address any legacy issues identified in prior safety

Enclosure

48

culture assessments (i.e., CAP report 0510074 and Synergy Safety Culture

Assessment) that impact the safety culture at PBNP. The executive summary,

analysis, and contemplated action plans shall also be submitted to the NRC.

5. By no later than December 31, 2008, NMC shall perform another survey at PBNP

comparable to the 2004 and 2006 surveys to assess trends of the safety culture at

the site and the overall effectiveness of corrective actions taken in response to prior

year assessments (i.e., CAP report 0510074 and 2006 Synergy survey).

6. By no later than 3 months after the receipt of the next cultural survey results at

PBNP, NMC shall submit the executive summary, analysis of the results, and the

contemplated corrective actions to the NRC.

7. NMC shall continue to implement a process which ensures that adverse employment

actions are in compliance with NRC employee protection regulations and principles

of SCWE.

8. In the event of the transfer of the operating license of any NMC operated facility to

another entity, the commitments shall survive for the NMC fleet generally and PBNP

specifically.

b.

Observations and Findings

The NRC performed the first inspection of the Confirmatory Order items in June 2007

and documented observations in IR 05000266/2007003; 05000301/2007003, Section

4OA2.3. Inspectors reviewed the licensees completion of Order Items 1, 2, and 3 and

identified several observations, which the licensee subsequently entered into the CAP as

AR 01096862.

The second NRC inspection was performed in June 2008 and documented in

IR 05000266/2008003; 05000301/2008003, Section 4OA5.2. Inspectors verified the

licensees corrective actions taken in response to the previous NRC observations,

documented in AR 01096862; reviewed the SCWE refresher and new supervisor training

program as required by Order Item 3; and reviewed the licensees actions in response to

Order Item 4. No issues were identified with the actions taken for Order Items 1 and 2,

and those two items were considered complete. Two Green findings

(NCV 05000266/2008003-11; 05000301/2008003-11 and FIN 05000266/2008003-12; 05000301/2008003-12) were identified by the inspectors for Order Items 3 and 4, those

items were not considered complete.

In July 2007, the PBNP operating license was transferred from the NMC to Florida

Power and Light (FPL) Energy Point Beach, LLC. In April 2009, FPL Energy Point

Beach, LLC changed its name to NextEra Energy Point Beach, LLC. Therefore, NextEra

Energy Point Beach, LLC assumed responsibility for compliance with the Order.

The status of the remaining open Order items is summarized below. Note that an item

status of complete refers to the status of the NRC review and inspection. Order Items 3,

7, and 8 contain ongoing actions that require continued implementation by the licensee.

(Complete) Order Item 3: The licensee continued implementation of Order Item 3, which

required, in part, that the licensee provide SCWE training to its employees holding

Enclosure

49

supervisory positions and higher. The inspectors reviewed AR 01129565, initiated for

NCV 05000266/2008003-11; 05000301/2008003-11, issued in 2008 when the

NRC inspection identified four individuals who did not meet the SCWE training

requirement. The four individuals who had exceeded the nine month requirement

specified in the Order were subsequently trained by the licensee. In the current

inspection, no additional supervisors were identified that missed the required training.

The inspectors attended SCWE training for supervisors and found the 2009 training

satisfactory. The inspectors reviewed the licensee procedures and the Learning

Management System and determined they were satisfactory to track personnel for the

required SCWE training, although the licensee recently identified several issues that

required additional corrective actions. The inspectors determined that these issues,

while not performance deficiencies, demonstrated that continued emphasis by the

licensee was warranted to preclude future performance issues. Some additional

oversight was provided by the plant training advisory board where, at the monthly

meetings, individual supervisors who required SCWE training were tracked.

(Complete) Order Item 4: The licensee has completed Order Item 4 concerning actions

resulting from the NMC 2004 and 2006 Comprehensive Cultural Assessments. On

March 29, 2007, the licensee submitted to the NRC an analysis of the 2006 culture

survey and the contemplated action plans (ML070890434). The inspectors verified that

the licensee conducted the focus group interviews with Priority 1 and 2 organizations to

understand the cause of the survey results, and that nuclear industry best practices were

reflected in the conduct of focus groups and action plans to address the issues at Point

Beach.

The inspectors reviewed the actions and status of the four "quick hitter" plans that were

identified as not complete in the 2008 NRC inspection and the basis for Finding 05000266/2008003-12; 05000301/2008003-12. The licensee addressed this deficiency

in AR 01129659 and the inspectors verified these "quick hitter" plans were complete.

The inspectors sampled several of the long-term actions plans and verified the licensee

completed those individual actions. However, the inspectors noted that the results of the

2008 safety culture survey (Order Item 5) revealed the overall composite site nuclear

safety culture rating remained low and the ratings from 2004 to 2008 showed minimal

improvement. Based on the NRC findings issued in 2008 and the results of the 2008

safety culture survey, the inspectors were concerned there was a lack of management

attention and priority to the action plans prior to the 2008 survey and that licensee

management did not recognize many of the actions taken were either not effective or

could not sustain improvements, especially in the departments which consistently had

the lowest survey result scores in the 2004, 2006 and 2008 surveys. Licensee actions

taken in response to the 2008 safety culture survey are discussed in the summary for

Order Item 5.

(Complete) Order Item 5: The licensee has completed Order Item 5, to perform another

survey at PBNP comparable to the 2004 and 2006 surveys. In June 2008, the licensees

contractor conducted a survey at Point Beach and submitted the results of the survey to

the NRC on December 22, 2008, (ML083660387). As previously noted in the Order

Item 4 discussion, the survey results did not show a marked improvement from the

2004/2006 surveys, and Point Beach continued to have an overall low nuclear safety

culture rating.

Enclosure

50

As a result of the 2008 survey, and because the licensee had exceeded three

assessment periods with a substantive cross-cutting issue in problem identification and

resolution, the licensee was requested by the NRC in the March 4, 2009,

Annual Assessment Letter to perform an independent assessment of the corrective

actions taken in response to the 2004, 2006, and 2008 culture surveys. The

independent assessment was performed from June 23 through June 25, 2009.

The inspectors determined that the assessment team, which consisted of four

individuals, was independent from the plant staff, with two members from FPL corporate,

one member from another utility company, and one member from a consultant company.

The inspectors noted that the assessment included personnel interviews, meeting

attendance, and document reviews. The licensees assessment concluded overall that

the corrective actions taken for the 2008 survey results were more effective than those

taken for the 2004 and 2006 culture surveys, and provided assurance that the progress

could be sustained. However, the inspectors noted that the report did not include any

detailed analysis or quantitative data as the basis for the assessments conclusions;

therefore, the inspectors could not evaluate the assessment teams conclusions. The

licensees assessment contained six observations and recommendations for

improvements which were:

an over-reliance on senior managements actions to establish expectations and

demonstrate desired safety culture behaviors; therefore, the team recommended

those behaviors be driven down to the department managers and line

organization;

while there is a high level of confidence in the CAP among licensee staff when

dealing with safety-related, industrial safety, or plant reliability issues, the same

confidence level does not exist with lower level issues, especially those which

are closed to trend; therefore, the team recommended supplemental trending

measures needed to be developed prior to the establishment of a fleet-trending

program;

while the managers interviewed understood safety culture, those same managers

could not clearly articulate a consistent picture of an excellent nuclear safety

culture; therefore, the team recommended that additional actions be taken to

ensure the management team could clearly articulate the description of an

excellent nuclear safety culture;

the safety culture effectiveness assessments were currently compliance-focused

with regard to the completion of corrective actions taken in response to the

culture surveys; therefore, the team recommended an effectiveness assessment

be performed to reevaluate the expectations provided in September 2008 and to

promote the day-to-day implementation of the core nuclear safety culture values;

the organization had difficulty separating day-to-day work place issues from

nuclear safety culture issues; therefore, the team recommended addressing

day-to-day work place issues in a different forum; and

one of the major focus areas from the 2008 culture survey was achieving a better

balance between workload and available resources, with the extended power

uprate project adding additional workload to the plant; therefore, the team

recommended the extended power uprate project should look for more effective

means of implementation, to avoid unnecessary disruptions of the normal plant

work schedule.

Enclosure

51

The independent assessment recommendations were entered into the CAP system as

AR 01152228.

The inspectors also reviewed a sample of the corrective actions taken for the

weaknesses identified in the 2008 safety culture survey and interviewed personnel in the

groups having the lowest ratings in the survey. Many of the licensee personnel

interviewed in December 2009 were interviewed during the 2007 and/or 2008 NRC

inspections. The inspectors observed that many of the actions were recently completed

and some groups made significant improvement, while other groups have shown

marginal improvement, if any. However, the inspectors noted that the Point Beach

Nuclear Safety Culture Improvement Team (NSCIT) developed and issued SCWE

performance indicators for all work groups and that those indicators reflected that some

groups remained as outliers (needed improvement). Those indicators aligned with the

NRC observations from day-to-day resident inspections and interviews conducted with

licensee personnel during this inspection.

In addition, the inspectors reviewed the results of other surveys performed on aspects of

safety culture by FPL in late 2008 and one performed by an independent organization

made up of external utility representatives in early 2009. While the inspectors concluded

that those surveys were not comparable to the licensees safety culture surveys

previously discussed, the inspectors noted that both surveys contained positive results

related to the nuclear safety culture and safety conscious work environment at

Point Beach, indicative of some improvement since the 2008 safety culture survey.

Therefore, the inspectors concluded that the safety culture environment has shown

some improvement and further monitoring by the plant NSCIT and continuing actions

from the safety culture surveys and independent assessment team recommendations

would be needed to continue this trend.

(Complete) Order Item 6: The licensee completed Order Item 6 when the licensee

submitted the 2008 Safety Culture Survey executive summary, analysis of the results,

and the contemplated corrective actions to the NRC on December 22, 2008,

(ML083660387). The inspectors verified these submittals were complete within the

timeframe contained in the Order.

(Complete) Order Item 7: The licensee continued implementation of Order Item 7 to

implement a process that ensured adverse employment actions were in compliance with

NRC employee protection regulations and principles of SCWE. The FPL Nuclear

Division Policy, NP-413, was put in effect on May 15, 2008, and replaced the

NMC procedure CP-0087. However, the inspectors observed that the FPL procedure

was not as detailed as the original NMC procedure, and a follow-up inspection would be

needed to look at specific adverse action cases. The licensee captured the inspectors

observations in condition report AR 01163410.

In a follow-up inspection, the inspectors reviewed a sample of adverse actions taken at

PBNP since policy NP-413 was implemented to ensure the Order requirements were

maintained. The inspectors also reviewed a new FPL Policy, HR-AA-01, Involuntary

Termination or Other Significant Employment Actions Affecting Nuclear Division

Employees, issued as a result of the inspectors previous observations. This new policy

contained the employee protection criteria that were missing from the previous policy.

During review of a sample of 10 adverse actions, the inspectors identified that in one

Enclosure

52

case the licensee had not completed an independent review of the personnel action by

the Human Resources Department as required by the policy. The licensee entered this

performance deficiency into the CAP as AR 01165164, performed the independent

review, and determined there were no employee protection issues involved. The

inspectors agreed with this determination and concluded the failure to implement the

FPL Policy was considered a minor violation, in accordance with the NRCs Enforcement

Policy.

(Complete) Order Item 8: For Order Item 8, the inspectors verified that after the transfer

of the operating license of PBNP from NMC to NextEra Energy (formerly FPL),

PBNP continued to follow the Order commitments.

No findings of significance were identified during this inspection.

Based on the results of this inspection and the actions documented in IRs

05000266/2007003; 05000301/2007003 and 05000266/2008003; 05000301/2008003,

the inspectors concluded that the licensee had implemented all the actions required by

the Confirmatory Order (EA-06-178). Therefore, the inspectors considered the

associated Apparent Violation 05000266/2006013-05; 05000301/2006013-05,

"Confirmatory Order EA-06-178," closed.

.5

Plant Modifications in Support of Extended Power Uprate (EPU) (71004)

a.

Inspection Scope

From November 30 through December 18, 2009, the inspectors reviewed the following

completed plant modifications during a baseline inspection for Evaluations of Changes,

Tests, or Experiments and Permanent Plant Modifications. The following two

modifications were completed for the Extended Power Uprate project, hence may be

also be credited as samples towards completion of IP 71004, Power Uprate. Additional

details of these samples are included in IR 05000266/2009007; 05000301/2009007.

Mechanical tie-ins to the SW and AFW systems for the new Unit 2 motor-driven

AFW pump. Specifically, the inspectors reviewed a sample of the associated

engineering change documentation, including the 10 CFR 50.59 screening,

design calculations, work orders, engineering change requests, and corrective

action documents, to assure the installed plant change was consistent with the

design and licensing bases. The inspectors walked down the mechanical tie-ins

to the SW and feedwater systems to verify the installed piping configurations

were consistent with the design and installation documentation.

Electrical and instrumentation tie-ins installed during the refueling outage for the

new Unit 2 motor-driven AFW pump per EC-13401. The inspectors walked down

changes to the Unit 2 control room panels with the SQUG engineer.

b.

Findings

No findings of significance were identified.

Enclosure

53

4OA6 Management Meetings

.1

Exit Meeting Summary

On January 5, 2010, the inspectors presented the inspection results to Mr. C. Trezise,

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed

was considered proprietary.

.2

Interim Exit Meetings

Interim exits were conducted for:

The Occupational Radiation Safety access control to radiologically significant

areas and ALARA program inspection results to Mr. L. Meyer and other members

of the licensee staff on October 30, 2009. This included closure of URI 05000266/2009004-01; 05000301/2009004-01 documented in Section 4OA5.

TI 2515/177 inspection results to Mr. L. Meyer and other members of the

licensee staff on October 30, 2009. The licensee acknowledged the issues

presented.

The ISI inspection results to Mr. L. Meyer and other members of the licensee

staff on November 6, 2009. The licensee acknowledged the issues presented.

The Verification of the Public Radiation Safety Performance Indicator inspection

results with Mr. J. Pierce on December 4, 2009.

The results of the Emergency Preparedness program inspection with

Mr. C. Trezise on December 11, 2009.

The licensed operator requalification training program inspection results with the

Training Operations Supervisor, Mr. R. Amundson, on December 15, 2009.

The annual review of Emergency Action Level and Emergency Plan changes

with the licensee's Emergency Preparedness Manager, Mr. R. Johnson, via

telephone on December 15, 2009.

The Confirmatory Order (EA-06-178) inspection results to Mr. L. Meyer and other

members of the licensee staff on December 18, 2009. The licensee

acknowledged the conclusions and observations presented.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary. Proprietary material received during the inspection was returned

to the licensee.

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Aerts, Accounting Manager (NSCIT Leader)

B. Castiglia, Performance Improvement Manager

J. Costedio, Nuclear Licensing Manager/Regulatory Affairs Manager

R. Farrell, Radiation Protection Manager

R. Freeman, Emergency Preparedness Manager

R. Harrsch, Operations Site Director

L. Hawkeye, Engineering PI Manager

C. Hill, Work Control Center Manager

P. Holzman, GL 89-13 Program Engineer

L. Meyer, Site Vice-President

J. Schroeder, SW System Engineer

C. Trezise, Engineering Director/Acting Site Vice-President

T. Vehec, Plant Manager

G. Vickery, Work Management Manager

Nuclear Regulatory Commission

M. Kunowski, Chief, Division of Reactor Projects, Branch 5

J. Poole, Point Beach Project Manager, Office of Nuclear Reactor Regulations

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened 05000266/2009005-01; 05000301/2009005-01

FIN

Failure to Meet GL 89-13 Program for Mussel Control

(Section 1R12.1)05000301/2009005-02

NCV Failure to Ensure Adequate Control of Foreign Material in

Safety-Related Systems (Section 1R15.1)05000301/2009005-03

NCV Failure to Update Safe Load Path Manual to Include

Safety-Related Cable Locations (Section 1R18.1)05000266/2009005-04; 05000301/2009005-04

URI

Potential Failure to Adequately Evaluate Seismic II/I

Concerns for Units 1 and 2 'B' Containment Sump Strainers

(Section 1R18.2)05000301/2009005-05

NCV Momentary Loss of Unit 2 Reactor Vessel Level Indication in

the Control Room (Section 1R20.1)05000266/2009005-06; 05000301/2009005-06

NCV Failure to Maintain Proper Control of Radioactive Material

Within the Radiologically Controlled Area (Section 4OA5.1)

2

Attachment

Closed 05000266/2009005-01; 05000301/2009005-01

FIN

Failure to Meet GL 89-13 Program Requirement for Mussel

Control (Section 1R12.1)05000301/2009005-02

NCV Failure to Ensure Adequate Control of Foreign Material in

Safety-Related Systems (Section 1R15.1)05000301/2009005-03

NCV Failure to Update Safe Load Path Manual to Include

Safety-Related Cable Locations (Section 1R18.1)05000301/2009005-05

NCV Momentary Loss of Unit 2 Reactor Vessel Level Indication in

the Control Room (Section 1R20.1)05000266/2009004-01; 05000301/2009004-01

URI

Failure to Control Radioactive Material Within the

Radiologically Controlled Area Resulting in Unnecessary

Dose to Worker (Section 4OA5.1)05000266/2009005-06; 05000301/2009005-06

NCV Failure to Maintain Proper Control of Radioactive Material

Within the Radiologically Controlled Area (Section 4OA5.1)05000266/2006013-05; 05000301/2006013-05

AV

Confirmatory Order EA-06-178 (Section 4OA5.4)

3

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the IR.

1R01 Adverse Weather Protection

- AR 00509533; O&MR 379; Revision 1 Freezing Of Instrumentation Piping

- AR 00509586; Reduced Pump Seal Life Because Of Improper Venting

- AR 01075828; PAB HV Steam Exhaust Stack Drain Line Is Frozen

- AR 01140416; Ice In Sealtite For Many Security Components

- AR 01140633; Beach Drains Frozen

- AR 01141214; Ice On Floor In Unit 1 Facade

- AR 01141395; EC 12789 Facade Freeze Upgrade DRB Action items

- AR 01141687; Verify Cold Weather Preps Remains In A Working Stat

- AR 01142302; U2 Facade Sump Piping Heat Trace Alarms

- AR 01142711; Inadequate 2X04 Cable Drip Tray Causes Ice Buildup In Facade

- AR 01142806; Changes To OI 106 To Incorporate EC 12789 Facade Freeze Mod

- AR 01143674; Faulted MUX Causing MET Tower Data To Be Frozen

- AR 01143775; Frozen Drain Line In Unit 2 Facade

- AR 01146740; Cold Weather Checks UNSAT - Heat Lamp GFI Tripped

- AR 01148041; Heat Trace Drawing Needs Updating

- AR 01148221; Facade Heat Trace Panel reliability Unsatisfactory

- AR 01148314; Heat Trace Drawing Needs Updating/More Information

- AR 00149677; Massive Formation Of Ice Has Collected On Cable Tray In Southwest Corner

Of Unit

- AR 01154068; Heat Trace For RS-SA-003 Installed Incorrectly

- AR 01155627; PC 49.5 Cold Weather Checklist, WH4 Heaters Broke

- AR 01155718; Heat Trace Not Installed Per Manufacturer Recommendations

- AR 01155829; Cold Weather Preps

- AR 01156747; Cold Weather Preps May Not Get Completed As Scheduled

- AR 01156940; Facade Freeze Tent

- AR 01156958; HV Piping Leak Downstream Of HV-990

- AR 01157478; CWPH MOD EC 11174 Requires Cold Weather Procedure Update

- AR 01158201; Cold Weather Issue - Primary And Backup Circuit In Alarm

- AR 01158202; Cold Weather Issue - Primary And Backup Circuit In Alarm

- AR 01158203; Cold Weather Issue - Vent To Atmosphere For RWST

- AR 01158938; Cold Weather Readiness System Engineering Reviews

- AR 01159535; BDE May Need Cold Weather Shutdown

- AR 01154813; Facade Freeze Protection Work Not Ready

- AR 01154683; Section Of Facade Heat Tracing Is Missing

- AR 01155829; Cold Weather Preps

- ICI 32; Facade Freeze Control Panel Settings; Revision 1

- IE Bulletin 79-24; Frozen Lines; September 27, 1979

- ISA-S67.02; Nuclear Safety-Related Instrument Sensing Line Piping And Tubing Standards

For Use In Nuclear Power Plants

- OP-AA-102-1002; Seasonal Readiness; Revision 0

- OM 3.39; Degraded Equipment / Adverse Condition Monitoring Procedure; Revision 2

4

Attachment

- 0-SOP HT-1B01; Unit 1 Non-Vital Train A Heat Trace Panels; Revision 0

- OM 3.9; Watchstation Status Checks And Watchstander Turnover Guides; Revision 15

- OI 106; Facade Freeze Protection; Revision 26

- OP-AA-102-1002; Seasonal Readiness; Revision 0

- PC 49; Cold Weather Preparations; Revision 7

- PC 49 Part 5; Cold Weather Checklist: Outside Areas And Miscellaneous; Revision 25

- WO #353856-07; Install 2FF-07-02C Heat Trace Cable On RS-SA-003 And Test

- WO #366472; 2VNTB-04802A Damper Not Fully Closing

- Drawing 019193; Electrical Layout Facade Area E-142; Unit 1

- Drawing 55805; Wiring Diagram Heat Tracing Panel "AH"; Auxiliary Building; Units 1 And 2

- Drawing 325073; Facade Freeze Protection Control Panel 1FFCP-02B; Secondary Distribution

Breaker Panelboard 1FFDP-02-5; Unit 1

- Generic Letter 88-20; Supplement 5; Individual Plant Examination Of External Events For

Severe Accident Vulnerabilities

1R04 Equipment Alignment

- 2-SOP-RH-002; Residual Heat Removal System Operation; Revision 3

- CL 7A; Safety Injection System Checklist Unit 2; Revision 30

- CL 7B; Safety Injection System Checklist Unit 2; Revision 27

- IT 04F; 2P-10A LHSI Pump Profile Test Mode 6 High Cavity Water Level Unit 2; Revision 4

- O-TS-EP-001; Weekly Power Availability Verification; Revision 11

- OP 7A; Placing Residual Heat Removal System In Operation; Revision 45

- Drawing ISI-2122; Residual Heat Removal Suction From Loop "A"; Unit 2

- Drawing ISI-2123; Residual Heat Removal Suction Header; Unit 2

- Drawing ISI-2125; Residual Heat Removal To Loop "B"; Unit 2

- Drawing ISI-2204; Residual Heat Removal Heat Exchangers HX-11A And HX-11B; Unit 2

- Drawing ISI-2228; Residual Heat Removal Pump Discharge; Unit 2

- Drawing ISI-2231; Residual Heat Removal Heat Exchanger Bypass; Unit 2

- Drawing ISI-PRI-2131; Residual Heat Removal To RPV; Unit 2

- Valve And Component Map; Pipeway 3; EL 8" PAB; Revision 0

- Valve And Component Map; Unit 2 RHR Heat Exchanger Cubicle; EL 5' PAB; Revision 4

- Valve And Component Map; Pipeway 3; Hallway Outside; EL 8' PAB; Revision 2

- Valve And Component Map; U2C - 46'; Revision 2

- Valve And Component Map; Unit 2 Containment; 10' And 21' Elevation; Revision 2

- Valve And Component Map; U2 A S/G Handhole Level; Area 2C-8; Revision 2

- Valve And Component Map; Unit 2 Containment "A" 10' Platform; Revision 3

1R05 Fire Protection

- FEP 4.0; Fire Emergency Plan; Revision 5

- FEP 4.20; Site; Revision 7

- FEP 4.26; North Service Building; Revision 3

- FHAR FZ245; Fire Area A01-E; Electrical Equipment Room - Unit 1; Fire Zone Data

- FHAR FZ775; Fire Area A71; G-04 Diesel Room; Fire Zone Data

- FOP 1.1; Brigade Training; Revision 9

- NP 1.9.14; Fire Protection Organization; Revision 10

- PC 74; Conducting And Evaluating Fire Drills; Revision 10

- Drawing 290590; Fire Protection For Turbine Building, Auxiliary Building And Containment;

Elevation 44' - 0"

- Shift Staffing Report; Station Log; Mid-Shift; December 10, 2009

5

Attachment

1R06 Flood Protection Measures

- AOP-9A; Service Water System Malfunction; Revision 24

- FSAR Appendix A.7; Plant Internal Flooding

- NP 8.4.17; PBNP Flooding Barrier Control; Revision 10

1R08 Inservice Inspection Activities

- AR 01142750; U2R30 Inservice Inspection

- AR 01160164; Delays In RPV Examinations

- AR 01153595; EPRI Issued Document For Dissimilar Metal Weld UT Exams

- AR 01144460; WCAP-15666-A (Reactor Coolant Pump Flywheel Examinations)

- AR 01125657; OE26445 - Nondestructive Examination Results Affect Core

- NDE-163; Manual Ultrasonic Examination Of Ferritic Pressure Vessel Welds Greater Than 2

Inches In Thickness; Revision 14

- NDE-109; Manual Ultrasonic Examination Using Longitudinal-Wave Straight-Beam

Techniques; Revision 8

- NDE-171; Manual Ultrasonic Examination Of Nozzle Inside Radius Sections; Revision 13

- NDE-451; Visible Dye Penetrant Examination Temperature Applications 45°F TO 125°F;

Revision 25

- NDE-753; Visual Examination (VT-2) Leakage Detection Of Nuclear Power Plant Components;

Revision 15

- NDE-757; Visual Examination For Leakage Of Pressure Vessel Penetrations; Revision 7

- AM 3-31; Alloy 600 Management Program; Revision 4

- Work Order Package 00352519; Replacement Of An ASME Section III, Class 1, RCS

To P-10A/B Residual Heat Removal Pump Suction Header Drain Valve 2RH-D-9

- Work Order Package 00352831; Replacement Of An ASME Section III, Class 1, Excess

Letdown Heat Exchanger 2HX-4 Outlet Drain Valve 2CV-D-11

1R11 Licensed Operator Requalification Program

- OP 1B; Reactor Startup; Revision 60

- OP 1C; Startup To Power Operation Unit 2; Revision 15

- Results Of Licensed Operator Annual Operating Tests; 2009

1R12 Maintenance Rule Implementation

- AM 3-4; Implementation Of The Maintenance Rule At PBNP; Revision 7

- AR 01157305; Delayed Inspection Raises GL 89-13 Program And CCW Questions

- AR 01159196; 2HX-015D Containment Fan Coolers Blocked With Mussels

- NAP-407; Equipment Reliability; Revision 5

- NP 7.7.4; Scope And Risk Significant Determination For The Maintenance Rule; Revision 17

- NP 7.7.5; Maintenance Rule Monitoring; Revision 21

- NP 7.7.7; Maintenance Rule Periodic Evaluation; Revision 4

- SEM 4.2; Component Maintenance Program Guideline; Revision 4

- Evaluation Of Exceeding The Assumed Value For Partially Blocked Flowpaths For The

Inspection Of Containment Fan Cooler 2HX-015A (EC14792)

- Evaluation Of Exceeding The Assumed Value For Partially Blocked Flowpaths For The

Inspection Of Containment Fan Cooler 2HX-015C And 2HX-015D (EC14793)

- Point Beach GT System Corrective Action Plan; Revision 0 and 1

- Point Beach SE-0401 Action Tracking Data; Gas Turbine AR/CAPs

6

Attachment

- Point Beach Gas Turbine System Health Report - Third Quarter 2009

- Point Beach Third Quarter System Matrix; July 1 - September 30, 2009

- Point Beach Fourth Quarter System Matrix; October 1 - December 31, 2009

- Point Beach Smart System Status Report; Gas Turbine System; December 15, 2007

- Point Beach Smart System Status Report; Gas Turbine System; January 17, 2008

- Point Beach Smart System Status Report; Gas Turbine System; February 28, 2008

- Point Beach Smart System Status Report; Gas Turbine System; May 2, 2008

- Point Beach Smart System Status Report; Gas Turbine System; August 1, 2008

- Point Beach Smart System Status Report; Gas Turbine System; January 1, 2009

- Point Beach Smart System Status Report; Gas Turbine System; February 23, 2009

- Point Beach Nuclear Plant Maintenance Rule (a)(1) Action Plan Timeline Data

- Point Beach Nuclear Plant Maintenance Rule Unavailability Data Sheet;

June 1, 2009 - November 1, 2009

- GL 89-13 Program Document; Revision 8

- Procedure AM 3-19; Biofouling Control Program; Revision 4

- Procedure OI 155; Chemical Treatment of Service Water for Mussels; Revision 27

- Calculation 2002-0008; CCW HX Plugging Limit; Revision 3

- AR 01158115; Unexpected TSAC Entry due to low accident cooler SW flow

- AR 01158344; 2HX-12D CC HX Found to be Approximately 66% blocked

- AR 01159196; 2HS-1015D Containment Fan Cooler Blocked with Mussels

- AR 01159293; Significant Number of Blocked Tubes on 2HX-15C CFC

- AR 01159787; HX-12C CCW HX Exceeds Allowed Blocked Tubes

- AR 01159890; Tubes Blocked in 2HX-12D

- AR 01160350; U2 "A CFC Exceeded Plugging Limits per Calculation 2002-0003

- EC14794; Evaluation of the Effect of the Blocked Flowpaths Found during the Inspection of

HX-12C and 2HX-12D; December 10, 2009

- HX-12C BIO/SILT Fouling Inspection Program Form, Inspection dated October 27, 2009

- HX-12D BIO/SILT Fouling Inspection Program Form, Inspection dated October 28, 2009

- HX-15C-6 BIO/SILT Fouling Inspection Program Form, Inspection dated October 22, 2009

1R13 Maintenance Risk Assessments and Emergent Work Control

- AR 01161450; Availability Of AFW Piping For Mode 5 Steam Generator Availability

- AR 01161450; Availability Of AFW Piping For Mode 5 Steam Generator Availability

- IN 95-35; Degraded Ability Of Steam Generators To Remove Decay Heat By Natural

Circulation

- NP 10.3.6; Shutdown Safety Review And Safety Assessment; Revision 30

- Control Room Log Entries Report; November 15 - 17, 2009

- Drawing 25494-200-M0K-0000-06061; Weld Map For FE-4036 Assembly

- Drawing 342215; ISI Isometric Auxiliary Feedwater To Steam Generator "B"

- Drawing 342217; ISI Isometric Auxiliary Feedwater To Steam Generator "A"

1R15 Operability Evaluations

- AR 01147224; Spent Fuel Pool Cooling Pump Was Rendered Non-Functional

- AR 01148036; P-12B Spent Fuel Pool Pump's RV Not Indicative Of True Performance

- AR 01156117; EPU Spent Fuel Pool Cooling Calculation Issues

- AR 01159196; 2HX-015D Containment Fan Coolers Blocked With Mussels

- AR 01160033; Apparent SW Leak; Unit 2 CFC HX-015A1-A4 Coils

- AR 01161636; New AFW Line In Contact With SW Pipe

- AR 01160007; Evidence Of Leakage From HX15A1-4

7

Attachment

- AR 01160262; 1HX-15C CFC Flow Out Of Limit Low Per TS-33

- AR 01160350; U2 "A" CFC Exceeded Plugging Limits Per Calculation 2002-0003

- AR 01160443; Found Washer Between Gasket And Flange Face On 2HX-15A3

- AR 01162022; Spent Fuel Pool Cooling System Incorrectly Classified

- AR 1159784; Spent Fuel Pool Pump Suction Isolation Valve Stem Contacting Adjacent Pipe

Insulation

- AR 1160262; 1HX-15C CFC Flow Out Of Limit Low Per TS-33

- CL 5C; Spent Fuel Pool Cooling And Refueling Water Circulating Pump Normal Operation

Valve Lineup

- DG-M09; Design Requirements For Piping Stress Analysis; Revision 2

- EN-AA-203-1001; Operability Determinations/Functionality Assessments; Revision 1

- NP 8.4.10; Exclusion Of Foreign Material From Plant Components And Systems;

Revisions 7 and 24

- TS 33; Containment Accident Recirculation Fan-Cooler Units (Monthly); Unit 1; Revision 31

- Causal Evaluation; 2SI-897B Failed To Operate (AR 1158812, AR1158797/WO 379810);

October 22, 2009

- Drawing 018993; Auxiliary Cooling System; Unit 1; Revision 44

- Drawing 018995; P&ID Service Water; Unit 1

- Point Beach Nuclear Plant A-46 Final Report; Introduction And Seismic Verification

Methodology; Revision 1

- Point Beach Nuclear Plant A-46 Final Report; Appendix A; Seismic Design For Structures and

Equipment

1R18 Plant Modifications

- 07 Calculation 2009-0022; Air Entrainment for Containment Sump Screens; 2009

- AR 01122278; Safe Load Paths For Turbine Building Crane

- AR 01145715; SLP 3 Revision 11 For Precautions Needed Over U2 Truck Bay

- CA 0112278; Safe Load Paths For Turbine Building Crane

- 10 CFR 50.59/72.48 Screening For CA 0112278; Safe Load Paths For Turbine Building Crane

- AR 01159514; 5B FWTR Heater Contacted And Damaged Component

- AR 01162492; ACE 01157505 Failed To Meet Minimum Requirements

- EC 11542; Unit 2 Main Generator Circuit Breaker Addition

- 10 CFR 50.59 Evaluation of EC 11542; Unit 2 Main generator Circuit Breaker Addition

- EC 12601; Additional Sump Strainer Modules - Unit 2; October 1, 2009

- EC 13601; GSI-191 RCP, S/G, and RCS Loops Piping Insulation Replacement - Unit 2;

February 11, 2008

- EC 14790; Validation of SSCs above the Unit 1 Sump B Suction Strainers; November 15,

2009

- EN-AA-203-1001; Operability Determinations/Functionality Assessments; October 8, 2009

- FSAR Appendix A.3; Control Of Heavy Loads

- MDB 3.2.5 1B30; 480 V AC Motor Control Centers; Unit 1; Revision 2

- MDB 3.2.6 2B30; 480 V AC Motor Control Centers; Unit 2; Revision 1

- OI 35B; Electrical Equipment General Information; Revision 14

- PASS 002452; Electrical Raceways - Unit 2 Containment 8ft; November 4, 2009

- PBNP Engineering Planning And Management Cable Schedule Data; Train "A" Cables

- PBNP U2R30 Draft Schedule (Fall 2009); September 2, 2009

- PBNP U2R30 Production Schedule; 72-Hour Look Ahead; October 18, 2009

- SCR 2009-0127-01; GSI-191 RCP, S/G, and RCS Loops Piping Insulation Replacement -

Unit 2; September 8, 2009

- SFS-PB2-GA-00; Sure-Flow Strainer Recirc Sump System Layout; February 18, 2009

8

Attachment

- SFS-PB2-GA-01; Sure-Flow Strainer General Notes; March 3, 2009

- SLP 3; Turbine Building Main Crane; Revisions 11 And 12-Draft A

- Bechtel Power Corporation Correspondence; Interim Load Paths For Safety-Related Handling

Devices; October 8, 1981

- Drawing 19739; Lighting Schedule Panel 7L; Revision 22

- Drawing 080034; P&ID Service Water; Unit 1; Revision 65

- Drawing 6704-E-151001; Diesel Generator Building Yard Area Grading Plan; Revision 4

- Drawing 6704-E-353403; Yard Area Diesel Generator Duct Bank Plan; Revision 5

- Drawing 82607-G1.0; Old FWH 5A And 5B Removal; Revision 1

- Drawing M-2007; Equipment Location - Plan; Ground Floor North; Revision 19

- Hatch Area Study Design; Truck Bay, Gantry Track, Door Position And Opening, A/B Train

Duct Banks

- Hatch Area Study With FWHTR Design; Truck Bay, Gantry Track, Door Position And Opening,

A/B Train Duct Banks Feedwater Heater With Plates

- Hatch Area Study With Plates Design; Truck Bay, Gantry Track, Door Position And Opening,

A/B Train Duct Banks With Plates

1R19 Post-Maintenance Testing

- AR 01159648; 2P-010B, Residual Heat Removal Pump Oiler Level Consumption

- AR 01160385; Bechtel Identification Of Precursors To EPC Contract

- AR 01160661; Failed Radiographs On Welds For EC11683

- AR 01161009; Failure Investigation Process Established Due To Repetitive Failure During

Radiographic Testing Of AFW Welds Associated With EC 133400

- AR 01161191; Bechtel Corrective Action Report Not Written As Required

- AR 01159839; Some Vent Valves Not Identified On Isometric Drawings (NRC-Identified)

- AR 01159862; Acceptance Criteria For Gas Voids May Be Incomplete (NRC-Identified)

- AR 01159937; Sump Strainer Ii/I Seismic Documentation Incomplete (NRC-Identified)

- AR 01163219; Lack Of Documentation To Support A Decision Of 2/1 Acceptability

(NRC-Identified)

- AR 01160941; No Requirement To Document Seismic II/I Evaluations; (NRC-Identified)

- AR 01158870; Found Badly Burned Contacts On 2B52-429K For Compressor K-4B

- AR 01159029; G-02 Foreign Material

- AR 01159056; Found G-02 Emergency Diesel Generator Start Lockout Relay 2 Out Of

Specification

- AR 01159161; 40 T Relay In G-02 Found Out Of Specification

- AR 01159187; Mis-Communication During Work Activity

- AR 01159410; Z-013 Main Hoist Has A Pinched Cable

- AR 01159721; Oil Addition To 2P-10B RHR Pump

- AR 01159843; Thermal Overloads Found Tripped On 2B52-329K

- AR 01159845; Minor Procedural Issues Encountered During G-02 PMT

- AR 01159960; 2P-010B Oiler Adjustment Mechanism Setup Improperly

- AR 01160179; 2P-10A RHR Pump Oiler May Be Incorrectly Installed

- AR 01160366; Low Flow Indication In OI 136A RHR "A" Train F & V

- AR 01160551; Inconsistent RHR Flow Limitations In Various Procedures

- AR 01160557; Discrepancies Found During NRC Observed IT-04A RHR Test

- AR 01160749; SLP-1 And -2 Conflict With OSHA Required Crane Checks

- AR 01161191; No Corrective Action Report Has Been Written To Document Trend Of Failed

Welds

- AR 01161192; Contrary to Requirement A 3-Inch Elbow Between Welds 44Q And 44M On

The Auxiliary Feed Water Project Was Cut Out Due To Being Deficient

9

Attachment

- AR 01161222; Site Evaluation Of NRC Information Notice 2009-20

- AR 01161691; Main generator Rotor(s) Weight Exceeds TB Crane (Z-14) Capacity

- AR 01161694; New Generator Rotor Weight Exceeds TB Crane (Z-14) Capacity

- AR 01161706; ASME B30.2 Code Year For Wire Rope Inspections

- AR 01161946; ACE 1160527 Not Accepted In A timely Manner

- AR 01162048; Load Block Leveler And White Substance On Wire Rope On Z-015

- AR 01162940; Work Orders Not Yet Completed From RCE

- IT 04A; RHR Pump And Valve Tests In DHR Mode (Cold Shutdown); Unit 2; Revision 26

- PI-AA-100-1002; Guideline For Failure Investigation Process; Revision 0

- 2-SOP-RH-002; Residual Heat Removal System Operation; Revision 3

- TS 3.7.5; Auxiliary Feedwater

- TS 82; Emergency Diesel Generator G-02 Monthly; Revision 77

- WO 376979; Replace Wire Rope On the Polar Crane; Unit 2

- Drawing 25494-200-M0K-0000-06061; Weld Map For FE-4036 Assembly; Revision 4

- Drawing 25494-200-M0K-0000-06062; Weld Map For 2FE-04036 Spool; Revision 1

- Drawing 25494-200-M0K-0000-06063; Weld Map For 2FE-4037 Assembly; Revision 6

- Drawing 25494-200-M0K-0000-06064; Weld Map For 2FE-4037 Spool; Revision 1

- Master Weld Log - Job No. 25494; Weld Map For 2FE-4037 Spool

- Point Beach Daily Quality Summary; November 12, 2009

- Point Beach U2R30 Outage Schedule; Polar Crane Cable Repair Data; October 25-26, 2009

- Polar Crane 2Z-013 Estimated Wire Rope Stretch Data

- Trico Manufacturing Corp; Technical Information Sheet; Effects Of Aeration On Constant Level

Oilers

- Trico Manufacturing Corp; Technical Information Sheet; Affects Of Air Movement On

Opto-Matic Oilers

- Trico Manufacturing Corp; Technical Information Sheet; Glass, LS, Or SS Opto-Matic Oilers

Instructions Before Installing

- Trico Manufacturing Corp; Technical Information Sheet; Opto-Matic Installation

- Trico Manufacturing Corp; Technical Information Sheet; Preventing Excessive Lubrication In

Oil Sump Applications

- Weld Failure Casual Evaluation; Aux Feed/Containment Spray Weld Failures;

November 14, 2009

1R20 Refueling And Other Outage Activities

- AOP-2B; Unit 2; Feedwater System Malfunction; Revision 15

- AR 01158914; Reactor Vessel Level Indication Wide Range Calculations On Hold

- AR 01160451; Add Transmitter Valving To I&C Pre-Outage Training

- AR 01161576; Unit 2 Reactor Heat Removal Components Will Exceed 125 Percent

- AR 01161998; Revise 535A To Better Document Full Stroke Manual Exercise Of 2RH-715C

- AR 01162196; Inservice Testing Program Acceptance Criteria

- AR 01162379; Unit 2, 2CC-738A Valve Did Not Go Full Shut

- ASTM Designation; A 193/A 193M-93a; Standard Specification For Alloy-Steel And Stainless

Steel Bolting Materials For High-Temperature Service

- ASTM Designation; B 16/B 16M-00; Standard Specification For Free-Cutting Brass Rod, Bar

And Shapes For Use In Screw Machines-EC 14895; 2RH-716A - Yoke Bushing Nut Bolt

Installation

- AR 01159071; Unable To Complete 21CP 04.024 Due To Mode Change

- AR 01159076; Unexpected Unit 2 Reactor Vessel High Alarm

- AR 01161058; PMT for RC-537 Not Performed According To Work Order Task

- AR 01161630; Cut Reinforcing Bar In AFW Pump Room Wall

10

Attachment

- AR 01161966; P-31B Discharge Elbow Support Degraded

- AR 01161994; Testing Of SG Atmospherics Prior To Mode 4

- AR 01162014; Issue With SG Atmospheric Testing In OP-1A

- AR 01162073; Duct Tape On 2MS-02020 Yoke And Gland Follower

- AR 01162088; 2MS-2015 Atmospheric Dump Stroke Time Exceeded IST Limit

- AR 91162106; 2FD-2608 HX-22B MSR BTV Stuck In Mid Position

- AR 01162110; 2AF-4006 Closed Light Continuity Not As Required

- AR 01162119; Lone Wire Laying On Floor Below Apron Section of 2C03

- AR 01162139; MOB-276 Tripping

- AR 01162146; Valve Contractor Missing Step Sign Offs

- AR 01162166; 2C-03 Control Board Indication Deficiencies

- AR 01162202; Mode Change Hold Process Improvement Suggestions

- AR 01162223; U2 Purge Spool Pieces Restrict Access To Valves

- AR 01162253; BALCM - Dried Boric Acid Found On Packing Gland - 2SI-V-09

- AR 01162316; Additive Valve Position Out-Of-Tolerance For GV 4

- AR 01162353; Feed Pump Seal Inlet Valve Frozen/Doesn't Move

- AR 01162379; Unit 2 2CC-738A Valve Did Not Go Full Shut

- AR 01163155; Ground Water Drain Line Dripping On U1F 6.5" Floor

- AR 01163605; Wrong Valves For Tubing And Valve Replacement For K-2b

- AR 01153633; 2Z-104B Needs Replacement

- CL 1B; Containment Barrier Checklist; Unit 2; Revision 58

- CL 2B; Mode 6 To Mode 5 Checklist; Revision 11

- CL 2C; Mode 5 to Mode 4 Checklist; Revision 15

- CL 2E; Mode 3 To Mode 2 Checklist; Revision 16

- CL 20; Post Outage Containment Closeout Inspection; Revision 19

- CR 99-2241; Need To Evaluate Implementation Of The Service Water Model To Ensure

Assumptions Are Valid

- EC 0014645; D-08 Battery Charger Temp Power From Alternate Source

- FP-E-MOD-02; Engineering Change Control; Revision 6

- FP-E-RTC-02; Equipment Classification - Q List; Revision 4

- IT 06; Containment Spray Pumps And Valves (Quarterly) Unit 2; Revision 61

- IT 45; Safety Injection Valves (Quarterly) Unit 2; Revision 51

- IT 45B; SI Valves (Shutdown) Unit 2; Revision 4

- IT 395; Safety Injection Valves (Annual) Unit 2; Revision 12

- NP 4.2.19; Entry requirements Into Various Radiologically Controlled Areas; Revision 16

- IWA-4000; Repair/Replacement Activities

- IWA-5000; System Pressure Tests

- IWB-5000; System Pressure Tests

- MR 97-102; RC Piping Overpressurization Relief - Unit 1; Final Design Description;

October 22, 1997

- OI 53; Positioning Of The Fuel Transfer Cart; Revision 12

- OP 1A; Cold Shutdown To Hot Standby; Revision 99

- OP 1B; Reactor Startup; Revision 61

- OP 1C; Startup To Power Operation; Unit 2; Revision 16

- OP5A; Reactor Coolant Volume Control; Revision 42

- 10 CFR 50.99/72.48 Screening For MR 97-102; RC Piping Overpressurization Relief - Unit 1

- RESP 4.1; BOL Physics Tests; Revision 24

- TRHB 10.2; Primary Systems Descriptions: Reactor Coolant System; Revision 9

- WO 00378956; 2RH-716A Yoke Bushing Nut Bolt Installation

- 10 CFR 50.59/72.48 Screening of WO 00378956; 2RH-716A Yoke Bushing Nut Bolt

Installation

11

Attachment

- 2-PT-RCS-1; Reactor Coolant System Pressure Test - Inside/Outside Containment; Unit 2;

Revision 3

- 21CP 04.023-1; Reactor Vessel Level Outage Calibration; Revision 7

- Calculation 2003-0057; Evaluation Of Service Water System Debris Transport To Auxiliary

Feedwater

- Control Room Log Entries Data; October 19-20, 2009

- Drawing 018941; Fuel Transfer Arrangement System 2224; Revision 6

- Drawing 018977; Auxiliary Coolant System; Unit 2

- Drawing 152353; Auxiliary Cooling System; Residual Heat Exchanger; Discharge To

Valve 720 To Loop B To Valve 742 To MOV 871 AC 601R-G; Unit 2

- Equipment Specification 677020; Fuel Transfer System; Revision 0

- NRC Generic Letter 88-17; Loss Of Decay Heat Removal 10 CFR 50.54(f); October 17, 1988

- Operations PCRA Backlog Scrub Data; December 23, 2009

- Point Beach AT-0246 Outage Action Request Mode Change Restraints Data;

December 3, 2009

- Pro-Line Water Screen Services, Inc.; Installation Of Lower Boot Flapper Seal And Main

Frame To Non-Metallic Basket Seals; September 12, 2001

- Rex Chainbelt Inc.; Conveyor And Process Equipment Division Service Manual; June 1965

- Unified Screw Threads Data; Table 3a - Coarse-Thread Series, UNC And UNRC - Basic

Dimensions; Table 3b - Fine-Thread Series, UNF And UNRF - Basic Dimensions

1R22 Surveillance Testing

- AR 00151138; OSHA Required Crane Inspection Not Performed

- AR 01158712; Possible Discrepancies Noted During 2Z-13 Visual Inspection

- AR 01158730; 2Z-013 Visually Indeterminable Lateral Support Connections

- AR 01158949; 2Z-013 Polar Crane Inspection Weaknesses

- AR 01159254; 2Z-013 Polar Crane Inspection Weaknesses

- AR 01159410; Z-013 Main Hoist Has A Pinched Cable

- ANSI B30.2.0 - 1976; Overhead And Gantry Cranes (Top Running Bridge, Multiple Girder)

- ASME B30.2-2001; Overhead And Gantry Cranes (Top Running Bridge, Single Or Multiple

Girder, Top Running Trolley Hoist)

- ASME B30.2-2005; Overhead And Gantry Cranes (Top Running Bridge, Single Or Multiple

Girder, Top Running Trolley Hoist)

- ASME OM CODE-1995; Code For Operation And Maintenance Of Nuclear Power Plants

- AR 01158563; Unit 2 Containment Polar Crane Trolley Failure To Move

- AR 01158730; 2Z-013 - Visually Indeterminable Lateral Support Connection

- AR 01158746; Unit 2 Z-13 Crane #1 Controller Bridge Control Broken

- AR 01158788; 2RMP 9118-1 Emergent Issuance

- AR 01159790; Polar Crane Stopped Working

- AR 01159794; Potential Improvement To PBV-9240

- AR 01160749; SLP-1 And -2 Conflict With OSHA Required Crane Checks

- AR 01160844; Outdated Daily Crane Inspection Form Used

- AR 01162152; 12L-25 Lighting Panel Breaker Found Tripped

- AR 01162165; AR Not Initiated For Adverse Condition

- AR 01162167; DC Ground Found During ORT 3A

- AR 01162172; D-09 AC Input Breaker Tripped

- AR 01162173; Sliders Found Open During RF-445

- AR 01162177; G-01 Alarms Received During ORT 3A

- AR 01162205; Use Of CAPs Not Reinforced In ORT 3A

- AR 01162206; SA-51 Interstage Bleed On K-3B SA Compressor Does Not Work

12

Attachment

- AR 01162212; Unexpected Alarm, 2C20A 2-2, D-01/D-03 DC Bus Under Voltage

- AR 01162222; Full Shut 2MS-5958 Indicates 12% Open Locally During ORT-54

- AR 01162638; 2DT-2081 Gasket Failure

- AR 01162668; 2P029T Oil Sample Contained Water

- AR 01162712; 2MS-2082 Trip Valve Leakage Observed During IT 09A

- AR 01162728; TS-81 G-01 EDG Testing While 2P-29 TDAFW Pump OOS

- AR 01162762; OBD Completion Did Not Reverse Changes To Procedure

- CMP 11.1; Component Maintenance Program; Revision 0

- FSAR Appendix A.3; Control Of Heavy Loads

- IT 09A; Cold Start Of Turbine-Driven Auxiliary Feed Pump And Valve Test (Quarterly) Unit 2;

Revision 49

- ORT 3A; Safety Injection Actuation With Loss Of Engineered Safeguards AC (Train A)

- NRC Correspondence To Wisconsin Electric Power Company; February 1, 1982

- NUREG-0612; Control Of Heavy Loads At Nuclear Power Plants

- 2RMP 9118-1; Containment Building Crane OSHA Operability Inspections; Revision 5

- SLP 10; Load Weight Listings And Rigging Figures; Revision 22

- WO 359117; Wire Rope Inspection

- ALPS Wire Rope Corporation; Certificate Of Conformance; October 25, 2009

- Control Room Log Entries Data; TDAFW Test; December 4 - 11, 2009

- Drawing 275460; Auxiliary Feedwater System Units 1 and 2

- Point Beach Nuclear Plant Wire Rope Inspection Criteria Instructions

- Priority Work Schedule Data; September 10, 2009

1EP2 Alert and Notification Evaluation

- ENS Notification 45553; Notification Due To A Single Emergency Siren Actuation;

December 9, 2009

- EPMP 6.0; Alert And Notification System; Revision 9

- FEMA Prompt Alert And Notification System Approval Letter And Design Report;

December 7, 1987

- PBNP ANS Maintenance Records; October 2007 - November 2009

- AR 01162916; Power Outages Caused Sever Sirens Out-of-Service Due To Weather

- AR 01160553; Replaced Siren P-013 Antenna

- AR 01130759; Siren Test Postponed Due To Severe Weather

1EP3 Emergency Response Organization Augmentation Testing

- EP 5.0; Organizational Control Of Emergencies; Revision 52

- EPIP 1.1; ERO Notification; Revision 56

- EPG 1.0; Point Beach Nuclear Plant Shift Augmentation Drill Guideline; Revision 13

- EPMP 7.0; Emergency Response Organization Notification System; Revision 6

- PBN EP TP; Emergency Preparedness Training Program Description; Revision 8

- Emergency Response Organization Training Drill Team Roster; December 3, 2009

- LMS ERO Qualification Status Verification; December 10, 2009

- NPM 2008-0130; March 27, Quarterly ERO Augmentation Drills;

May 2, 2008 - September 17, 2009

- AR 01162982; Augmentation Drills Taking Credit For 30-Minute Chemistry Technician With

On-shift Chemistry Technician

- AR 01162977; Augmentation Drill Start Time Questioned During NRC Inspection

- AR 01162972; Loss Of Dialogics ERO Notification System Capabilities

- AR 01155763; EP ERO Expectations For Wearing A Pager

13

Attachment

- AR 01153790; July 28, 2009 Drill Dose Assessment Challenge

- AR 01156706; September 17, 2009 Augmentation Drill Two Responders Greater Than

30 Minutes And One Responder Greater Than 60 Minutes

- AR 01151489; June 16, 2009 ERO Augmentation Drill Two Responders Greater Than

30 Minutes

1EP4 Emergency Action Level And Emergency Plan Changes

- EP 2.0; Emergency Plan Acronyms And Definitions; 41 and 42

- EP 6.0; Emergency Measures; 50, 51, and 52

- EPIP 1.2.1; Emergency Action Level Technical Basis; 3

- 10 CFR 50.54(q) Reviews For Emergency Plan And EAL Revisions

1EP5 Correction Of Emergency Preparedness Weaknesses And Deficiencies

- Focused Self-Assessment Report PBSA-EP-09-03; Point Beach Emergency Preparedness

Pre-NRC Inspection; November 3, 2009

- Point Beach Toxic Gas Unusual Event July 3, 2008 Report; July 14, 2008

- Point Beach Security Unusual Event April 8, 2008 Report; May 7, 2008

- Point Beach Loss Of Off-Site Power Unusual Event January 15, 2008 Report;

February 26, 2008

- PBNP 09-026; Emergency Preparedness Audit; August 12, 2009

- PBNP 08-026; Emergency Preparedness Assessment; August 12, 2008

- PBNP 08-011; Emergency Preparedness Assessment; May 3, 2008

- AR 01151074; EPlan Organization Chart Different Than Site Organization Chart

- AR 01149526; Radiation Protection Leader Position Drops Below Three Deep

- AR 01136999; Self-Assessment DEP Data Discrepancy

- AR 01131429; July 3, 2008 Evaluate Toxic Gas EAL

- AR 01131394; July 3, 2008 Unusual Event

- AR 01121253; Transfer Of Command And Control Confusion During January 15, 2008

Unusual Event

- AR 01120314; Unusual Event January 15, 2008 ENS Notification Made At 59 Minutes

2OS1 Access Control to Radiologically Significant Areas

- RWP 00000861, Fuel Motion And Sent Fuel Pool Activities; Revision 1

- HP 2.14; Containment Keyway Personnel Access; Revision 15

- HP 2.15.1; High Level Contamination And Discrete Radioactive Particle Control; Revision 5

- HP 2.17; Very High Radiation Area Personnel Access; Revision 7

- HP 2.6; Locked And Very High Radiation Area Key Control; Revision 32

- HP 3.2; Radiological Labeling, Posting And Barricading Requirements; Revision 50

- HP 3.2.10; Secure High Radiation Area Controls; Revision 1

- HP 3.6; Alpha Monitoring Program; Revision 0

- HPIP 1.64; Control of Underwater Diving In Radiologically Hazardous Areas; Revision 7

- HPIP 2.1.1; Response Checks Of Portable Survey Instruments; Revision 11

- HPIP 3.50; Radiation Surveys; Revision 13

- FP-RP-JPP-01; Radiation Protection Job Planning; Revision 6

- 0-SOP-FH-001; Fuel/Insert/Component Movement In the Spent Fuel Pool Or New Fuel Vault;

Revision 15

- RP 1C, Refueling; Revision 65

- RP 2A; Receipt Of New Fuel Assemblies; Revision 47

14

Attachment

- RP-18 Part 3; Place Loaded DSC/TC Back Into The Spent Fuel Pool; Revision 3

- RESP- 2.3; Defective Removable Top Nozzle Replacement; Revision 7

- HPCAL 1.1; Radiation Protection Instrument Calibration, Repair And Response Checks;

Revision 22

- NP 4.2.19; Entry Requirements Into Various Radiologically Controlled Areas; Revision 16

- NP 4.2.32; Respiratory Protection Program; Revision 7

- AR SAR 01142742; Access Control To Radiologically Significant Areas And ALARA Planning

And Controls

- AR SAR 0115197; Access Control To Radiologically Significant Areas And ALARA Planning

And Controls

2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls

- FP-WM-PLA-01; Work Order Planning Process; 5

- NP 4.2.1; ALARA Program; Revision 20

- FP-RP-JPP-01; RP Job Planning; Revision 6

- FP-RP-RWP-01; Radiation Work Permit; Revision 8

- Radiological Controls And Associated ALARA Files For Insulation; Work Orders 00371055,

00371056, And 00371057

- Radiological Controls And Associated ALARA Files For RCP Work; Work Orders 00356469,

00358775, And 00366298

- Radiological Controls And Associated ALARA Files For Core Barrel Move; Work Order 00365421

4OA1 Performance Indicator Verification

- 2-PT-AF-2; Turbine Driven Auxiliary Feedwater System And MS Supply Pressure Test Outside

Containment - Unit 2

- AR 01135651; AF Mod Deferral Requires MSPI Basis Document Update

- AR 01138122; PRA Change For MSPI Not Explained In Submittal File

- AR 01138400; PRA Change For MSPI Not Explained In Submittal File

- AR 01142718; MSPI Margin Reduced Due To PRA Change

- EPG 1.1; Performance Indicator Guideline; Revision 6

- EPMP 6.0; Alert And Notification System Siren Function Data; October 2008 -

September 2009

- FG-E-MSPI-01; Mitigating System Performance Index; Revision 3

- LI-AA-200-1000-10000; FPL Fleet Licensing Performance Indicators; Revision 00

- Mitigating Systems Performance Index (MSPI) Basis Document Data For Point Beach Nuclear

Plant; Revisions 12 And 14

- MSPI Monthly Unavailability And Verification Data; July, August, And September, 2008

- MSPI Monthly Unavailability And Verification Data; October, November, And December, 2008

- MSPI Monthly Unavailability And Verification Data; January, February, And March, 2009

- MSPI Monthly Unavailability And Verification Data; April, May, And June, 2009

- NP 5.2.16; NRC Performance Indicators; Revision 14

- NRC Occupational Exposure Performance Indicator Data; October 2008 Through

September 2009

- Alert and Notification System Performance Indicator Records; October 2008 -

September 2009

- Atmospheric Effluent Radioisotopic Quantification Report; March 2009

- Atmospheric Effluent Radioisotopic Quantification Report; June 2009

- Atmospheric Effluent Radioisotopic Quantification Report; September 2009

15

Attachment

- Drill And Exercise Performance PI Results; October 2008 - September 2009

- Drill And Exercise Performance Records; October 2008 - September 2009

- ERO Drill Participation Summaries; December 2008 - September 2009

- ERO Participation Monthly Reports; December 2008 - September 2009

- Emergency Preparedness Attendance Reports; December 2008 - September 2009

- Liquid Effluent Radioisotopic Quantification Report; March 2009

- Liquid Effluent Radioisotopic Quantification Report; June 2009

- Liquid Effluent Radioisotopic Quantification Report; September 2009

- Mitigating Systems Performance Index Derivation Report Units 1 And 2; Heat Removal

System; Third Quarter of 2008 Through Second Quarter of 2009

- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 5

- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 6;

October 2009

- NP 1.10.1; Record Keeping For NRC Licensed Operators; Revision 8

- NP 5.2.16; NRC Performance Indicators; Revision 14

- NP 5.2.17; Equipment Performance And Information Exchange (EPIX); Revision 2

- OI 62A; Motor-Driven Auxiliary Feedwater System (P-38A And P-38B)

- TRHB 11.4; Secondary Systems Descriptions: Auxiliary Feedwater System; Revision 10

- Control Room Log Entries; July 2008 through June 2009

4OA2 Identification and Resolution of Problems

- AR 01114734; Lack Of Progress On Cable Submergence Issue

- AR 01163603; Trend Coding Of CAPS

- AR 01138519; FM Found During Lower Core Plate Inspection

- AR 01157789; FME Barrier Found Inside FW Heater 4A During Inspection

- AR 01158516; Component Cooling Water Heat Exchanger FME Issues

- AR 01158573; Wrench Dropped Into Cavity

- AR 01159958; Foreign Material Found In Discharge Of 2CV-257

- AR 01160348; FM Debris Scan Challenged RV Lower Internal Install (2R30)

- AR 01160355; LUVS Screen Dropped In Refuel Cavity

- AR 01160443; Found Washer Between Gasket And Flange Face On 2HX-15A3

- AR 01160489; Foreign Material On Lower Core Plate

- AR 01160494; Trend - Submerged Electrical Cables

- AR 01160572; Resource Needs Were Not Identified To Support FM Inspection In RMP

- AR 01160820; U2R30 Cavity Foreign Material Controls

- AR 01160980; SFMEA Concerns At The Spent Fuel Pool

- AR 01161181; Untimely Reporting Of foreign Material

- AR 01161214; Z-756 Hoist Pendant Damage Causes Hoist Inoperability

- AR 01161216; FME Found While Inspecting Portion Of 2A02 Bus

- AR 01161285; Sump Bravo Needs Fabricated FME Covers When Elbows Are Removed

- AR 01161310; During 2ICP 02.019 Testing, We Found A Hair In PC-949B-XA

- AR 01161672; Bechtel Contamination Control For Valves And Pipes

- AR 01162133; Foreign Material Found In The New Output Breakers

- AR 01162169; FME Issue Of Bottle Dropped In Stabrex Tanker

- AR 01162213; No Housing Covers Installed On FD Valve Operators

- AR 01162509; Four Absorbent Bags Found In the Unit 2 Turbine Hall Sump

- CMP 12.0; Equipment Failure Trending; Revision 5

- FG-PA-CTC-01; CAP Trend Code Manual; Revision 11

- FG-PA-DRUM-01; Department Roll Up Meeting Manual - Department Performance Trending;

Revision 8

16

Attachment

- PBN-09-010; Point Beach Nuclear Assurance Report; System Engineering; May 26, 2009

- REI 48.0; Reactor Engineering Trending Program; Revision 2

- Point Beach Nuclear Plant AT-0384 Activity Trending Data; December 21, 2009

- Point Beach Nuclear Plant Drum Summary Report; First Quarter 2009

- Point Beach Nuclear Plant Drum Summary Report; Second Quarter 2009

4OA5 Other Activities

- AR 01165164; NP-413 Policy Requirement Not Implemented

- Policy HR-AA-01; Involuntary Termination Or Other Significant Employment Actions Affecting

Nuclear Division Employees; Revision 0

- Policy SY-AA-02; Denial of Unescorted Access to FPL/FPLE Nuclear Facility; Revision 0

- FP&L NUC GET Plant Access Training 003; Revision Dated July 26, 2006

- HPIP 1.60; Calculating Shallow And Deep Dose Rates Due To Skin Contamination;

Revision 11

- NP 1.7.3; Site Specific Requirements For Access To And Termination From Point Beach

Nuclear Plant; Revision 18

- NP 4.2.25; Release Of Material, Equipment And Personal Items From The Radiologically

Controlled Areas; Revision 14

- Apparent Cause Evaluation - AR 01150045; Loss Of Radioactive Material Control Inside

Protected Area; Revision 1 and 2

- Chesapeake Nuclear Services Final Report, Dose Assessment For May 21, 2009

Contamination Event At The Point Beach Nuclear Plant; September 10, 2009

- Dispersed Contamination Dose Assessment Summary; July 2, 2009

- Personnel Contamination Event Report; May 21, 2009

- DRW 110E029, Sheet 1; Auxiliary Coolant System; September 10, 2008.

- DRW 110E035, Sheet 1; Safety Injection System; August 1, 2007

- DRW P-248; Residual Heat Removal System; December 25, 1999

- DRW P-237; SIS to Primary Coolant Cold Leg; January 22, 2004

- PO No. 00024065; Point Beach Walkdown Closure Report; November 16, 2009

- AR 01129366; PBNP Confirmatory Order Requirements Sustainability For Adverse

Employment Actions

- AR 01129462; Schedule For Incumbent Mgrs/Supv For NLA Course

- AR 01129565; 4 Individuals Not Meeting SCWE Confirmatory Order

- AR 01129659; EA 06-178 Confirmatory Order Inspection Finding

- AR 01152228; Independent Assessment Of The Effectiveness Of Corrective Actions From

Safety Culture Survey

- AR 01157190; Schedule PBN Personnel For SDA/LF Slots

- AR 01157534; Quick Hit Assessment PBSA-SRC-09-04

- AR 01162560; Security Supervisor Not Tracked For Required SCWE Training

- AR 01162564; 7 People Required To Attend SCWE Training And Not Being Tracked

- AR 01163410; Follow-up Issue SCWE Confirmatory Order Inspection

- FPL Nuclear Policy NP-413; Involuntary Termination of Division Employees; Revision 5

- NMC Policy CP 0087; Material Employment Action Review; Revision 0

- Corrective Action Effectiveness Review -AR01070153-12, April 29, 2009

- Memo from F. Flentje to J. Costedio; Verification of 2007 SCWE Confirmatory Order Actions

Committed During September, 24, 2008 Public Meeting with NRC; February 14, 2009

- PARB Presentation for Non-Performance of EFR 1070334, Adverse Employment Action

Policy, November 30, 2007

- Memo from B. Deuel to Nuclear Safety Culture Improvement Team; September 30, 2009

Nuclear Safety Culture Improvement Team Meeting Minutes; September 30, 2009

17

Attachment

- Memo from B. Deuel to Nuclear Safety Culture Improvement Team; December 2, 2009

Nuclear Safety Culture Improvement Team Meeting Minutes; December 2, 2009

- Memo from L Meyer to File; August 2009 PBNP PTAB Meeting Minutes; September 12, 2009

- Memo from L Meyer to File; February 2009 PBNP PTAB Meeting Minutes; February 23, 2009

- Point Beach Supervisor Leadership Development Program; Training Program Description;

Revision 6

- Point Beach Succession Plan; January 2010

- Point Beach Knowledge Retention Program; December 2009

- NRC 2007-0015, NMC Letter to NRC; NMC Plan to Address the Safety Culture Issues an at

Point Beach Nuclear Plant; March 29, 2007 (ML070890434)

- NRC 2008-0078, FPL Energy Letter to NRC; Status of Action Plans Taken in Response to

Confirmatory Order EA-06-178; November 11, 2008 (ML083170356)

- NRC 2008-0090, FPL Energy Letter to NRC; Confirmatory Order EA-06-178 Section IV.6

Nuclear Safety Culture Survey Results; December 22, 2008 (ML083660387)

- Point Beach Independent Assessment of Safety Culture Survey Corrective Action

Effectiveness; June 28, 2009

18

Attachment

LIST OF ACRONYMS USED

AC

Alternating Current

ACE

Apparent Cause Evaluation

ADAMS

Agencywide Document Access Management System

ADR

Alternative Dispute Resolution

AFW

Auxiliary Feedwater

ALARA

As-Low-As-Is-Reasonably-Achievable

ANS

Alert and Notification System

AOV

Air Operated Valve

AR

Action Request

ASME

American Society of Mechanical Engineers

AV

Apparent Violation

BACC

Boric Acid Corrosion Control

CAP

Corrective Action Program

CCWHX

Component Cooling Water Hear Exchanger

CFC

Containment Fan Cooler

CFR

Code of Federal Regulations

EA

Enforcement Action

EC

Engineering Change

EDE

Effective Dose Equivalent

ELHX

Excess Letdown Heat Exchanger

EP

Emergency Preparedness

EPRI

Electric Power Research Institute

EPU

Extended Power Up-Rate

ERO

Emergency Response Organization

FPL

Florida Power and Light

FSAR

Final Safety Analysis Report

FW

Feedwater

GL

Generic Letter

GSI

Generic Safety Issue

I&C

Instrumentation and Control

IEL

Initiating Event Likelihood

IMC

Inspection Manual Chapter

IP

Inspection Procedure

IR

Inspection Report

ISI

Inservice Inspection

LER

Licensee Event Report

LI

Level Indicator

LOCA

Loss of Coolant Accident

LOLC

Loss of Level Control

LOOP

Loss of Off-site Power

LT

Level Transmitter

mrem

Millirem

MSPI

Mitigating Systems Performance Index

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NMC

Nuclear Management Company

NRC

U.S. Nuclear Regulatory Commission

NSCIT

Nuclear Safety Culture Improvement Team

OSHA

Occupational Health and Safety Administration

19

Attachment

P&ID

Piping and Instrumentation Diagram

PARS

Publicly Available Records System

PBNP

Point Beach Nuclear Plant

PI

Performance Indicator

POS

Plant Operating State

PMT

Post-Maintenance Testing

PT

Pressure Test

RCA

Radiologically Controlled Area

RCS

Reactor Coolant System

RFO

Refueling Outage

RHR

Residual Heat Removal

RWP

Radiation Work Permit

RWST

Refueling Water Storage Tank

SCWE

Safety-Conscious Work Environment

SDP

Significance Determination Process

SG

Steam Generator

SI

Safety Injection

SLP

Safe Load Path

SQUG

Seismic Qualification Users Group

SRA

Senior Reactor Analyst

SW

Service Water

TI

Temporary Instruction

TS

Technical Specification

TSAC

Technical Specification Action Statement

TTB

Time-to-Boil

URI

Unresolved Item

VT

Visual Examination

WO

Work Order

L. Meyer

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records System (PARS) component of NRC's document

system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Michael Kunowski, Chief

Branch 5

Division of Reactor Projects

Docket Nos. 50-266; 50-301

License Nos. DPR-24; DPR-27

Enclosure:

IR 05000266/2009005; 05000301/2009005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServe

DOCUMENT NAME: G:\\1-Secy\\1-Work In Progress\\POI 2009 005.doc

Publicly Available

Non-Publicly Available

Sensitive

Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl

"E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

NAME

SOrth

MKunowski:cms

DATE

02/10/2010

02/10/2010

OFFICIAL RECORD COPY

Letter to L. Meyer from M. Kunowski dated February 10, 2010

SUBJECT:

POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED

INSPECTION REPORT 05000266/2009005; 05000301/2009005 AND STATUS

OF CONFIRMATORY ORDER EA-06-178

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