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{{Adams|number = ML083101203}} | {{Adams | ||
| number = ML083101203 | |||
| issue date = 11/05/2008 | |||
| title = IR 05000220-08-004 and 05000410-08-004; on 07/01/08 - 09/30/08; Nine Mile Point Nuclear Station, Units 1 and 2; Maintenance Risk Assessment and Event Followup (NRC Integrated Inspection Report) | |||
| author name = Dentel G T | |||
| author affiliation = NRC/RGN-I/DRP/PB1 | |||
| addressee name = Polson K J | |||
| addressee affiliation = Nine Mile Point Nuclear Station, LLC | |||
| docket = 05000220, 05000410 | |||
| license number = DPR-063, NPF-069 | |||
| contact person = Dentel, G RGN-I/DRP/BR1/610-337-5233 | |||
| document report number = IR-08-004 | |||
| document type = Inspection Report, Letter | |||
| page count = 38 | |||
}} | |||
{{IR-Nav| site = 05000220 | year = 2008 | report number = 004 }} | {{IR-Nav| site = 05000220 | year = 2008 | report number = 004 }} | ||
=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406-1415 November 5, 2008 | ||
Mr. Keith Vice President Nine Mile Point Nine Mile Point Nuclear Station, LLC P.O. Box 63 Lycoming, NY 13093 | Mr. Keith Vice President Nine Mile Point | ||
Nine Mile Point Nuclear Station, LLC | |||
P.O. Box 63 | |||
Lycoming, NY 13093 | |||
SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000220/2008004 and 05000410/2008004 | SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000220/2008004 and 05000410/2008004 | ||
==Dear Mr. Polson:== | ==Dear Mr. Polson:== | ||
On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Nine Mile Point Nuclear Station, Units 1 and 2. The enclosed integrated inspection report documents the inspection results discussed on October 24, 2008, with you and members of your staff. | On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an | ||
inspection at your Nine Mile Point Nuclear Station, Units 1 and 2. The enclosed integrated | |||
inspection report documents the inspection results discussed on October 24, 2008, with you and | |||
members of your staff. | |||
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. | The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. | ||
The inspectors reviewed selected procedures and records, observed activities, and interviewed | The inspectors reviewed selected procedures and records, observed activities, and interviewed | ||
personnel. | |||
This report documents one self-revealing finding and one NRC-identified finding of very low | |||
Sincerely,/RA/ Glenn T. Dentel, Chief Projects Branch 1 Division of Reactor Projects Docket No.: 50-220, 50-410 License No.: DPR-63, NPF-69 | safety significance (Green). One of the findings was determined to involve a violation of NRC | ||
requirements. However, because of its very low safety significance and because it was entered | |||
into your corrective action program (CAP), the NRC is treating this violation as a non-cited | |||
violation in accordance with Section VI.A.1 of the NRC's Enforcement Policy. If you contest the | |||
non-cited violation noted in this report, you should provide a response with the basis for your | |||
denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory | |||
Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to the | |||
Regional Administrator, Region I; the Director, Office of Enforcement; U.S. Nuclear Regulatory | |||
Commission, Washington, D.C. 20555-001; and the NRC Senior Resident Inspector at Nine Mile Point Nuclear Station. | |||
In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its | |||
enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Public ly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | |||
Sincerely,/RA/ Glenn T. Dentel, Chief Projects Branch 1 | |||
Division of Reactor Projects Docket No.: 50-220, 50-410 License No.: DPR-63, NPF-69 | |||
===Enclosure:=== | ===Enclosure:=== | ||
| Line 28: | Line 77: | ||
===w/Attachment:=== | ===w/Attachment:=== | ||
Supplemental Information cc w/encl: | Supplemental Information | ||
M. Wallace, Vice - Chairman, Constellation Energy H. Barron, President, CEO & Chief Nuclear Officer, Constellation Energy Nuclear Group C. Fleming, Esquire, Senior Counsel, Nuclear Generation, Constellation Energy Group, LLC M. Wetterhahn, Esquire, Winston & Strawn T. Syrell, Director, Licensing, Nine Mile Point Nuclear Station P. Tonko, President and CEO, New York State Energy Research and Development Authority J. Spath, Program Director, New York State Energy Research and Development Authority P. Eddy, New York State Department of Public Service C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law Supervisor, Town of Scriba P. Church, Oswego County Administator T. Judson, Central NY Citizens Awareness Network D. Katz, Citizens Awareness Network G. Detter, Manager, Nuclear Safety and Security, Constellation Energy | |||
cc w/encl: | |||
M. Wallace, Vice - Chairman, Constellation Energy | |||
H. Barron, President, CEO & Chief Nuclear Officer, Constellation Energy Nuclear Group | |||
C. Fleming, Esquire, Senior Counsel, Nuclear Generation, Constellation Energy Group, LLC M. Wetterhahn, Esquire, Winston & Strawn | |||
T. Syrell, Director, Licensing, Nine Mile Point Nuclear Station | |||
P. Tonko, President and CEO, New York State Energy Research and Development Authority | |||
J. Spath, Program Director, New York State Energy Research and Development Authority | |||
P. Eddy, New York State Department of Public Service | |||
C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law | |||
Supervisor, Town of Scriba | |||
P. Church, Oswego County Administator | |||
T. Judson, Central NY Citizens Awareness Network | |||
D. Katz, Citizens Awareness Network | |||
G. Detter, Manager, Nuclear Safety and Security, Constellation Energy | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
.............................. | IR 05000220/2008004, 05000410/2008004; 07/01/08 - 09/30/08; Nine Mile Point Nuclear Station, | ||
Units 1 and 2; Maintenance Risk Assessment and Event Followup. | |||
The report covered a three-month period of inspection by resident inspectors and regional specialist inspectors. One Green non-cited violation (NCV), and one Green finding, were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process (SDP)." | |||
Findings for which the SDP does not apply may be Green or be assigned a severity level after | |||
NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. | |||
===A. NRC-Identified and Self-Revealing Findings=== | |||
===Cornerstone: Initiating Events=== | |||
: '''Green.''' | |||
A self-revealing finding was identified on July 14, 2008, when inadequate maintenance practices, during replacement and troubleshooting of a Unit 2 radioactive waste sump pump, caused an electrical transient that resulted in the loss of numerous plant components and required a power reduction. The inadequate maintenance practices included failure to perform post-maintenance testing and continuation of troubleshooting despite having obtained results that were not consistent with the troubleshooting plan. This issue was entered into NMPNS's corrective action program for evaluation. | |||
The finding was greater than minor because it affected the human performance attribute of the Initiating Events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The finding was evaluated in accordance with IMC 0609 and determined to be of very low safety significance because the finding did not contribute to both the likelihood of a rector trip and the likelihood that mitigation equipment or functions would not be available, and did not screen as potentially risk significant due to external events. The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appropriately plan the pump troubleshooting activity by incorporating abort criteria (H.3.a per IMC 0305). (Section 4OA3) | |||
===Cornerstone: Mitigating Systems=== | |||
: '''Green.''' | |||
An NRC-identified non-cited violation (NCV) of 10 CFR 50.65(a)(4) was identified for inaccurate risk assessments completed for August 5 and 6, 2008. | |||
Specifically, the unavailable reactor core isolation cooling (RCIC) system was not properly incorporated into the risk assessment. The cause was determined to be that an error had been made while entering a change to the risk monitor computer software, which resulted in RCIC incorrectly being assigned a zero risk importance. | |||
As corrective actions, the modeling of RCIC was corrected and a verification of all mapping codes used in the risk monitor was performed. | |||
The finding was greater than minor because the risk assessment for RCIC system maintenance was inadequate due to inaccurate information that was provided to the risk assessment tool. As a result, the ov erall elevated plant risk, when correctly assessed, put the plant into a higher licensee-established risk category. The finding was evaluated in accordance with IMC 0609, Appendix K, and determined to be of very low safety significance because the incremental core damage probability deficit (ICDPD) was less than 1E-6. The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appr opriately plan work activities by incorporating valid risk insights (H.3.a per IMC 0305). (Section 1R13) | |||
===B. Licensee-Identified Violations=== | |||
None. | |||
5 | |||
=REPORT DETAILS= | =REPORT DETAILS= | ||
............ | |||
===Summary of Plant Status=== | |||
Nine Mile Point Unit 1 began the inspection period at full rated thermal power (RTP). Several | |||
short duration power reductions were performed for maintenance on reactor recirculation pump (RRP) motor-generators, and on September 27, power was reduced to 68 percent for a control | |||
rod sequence exchange, single rod scram time testing, and turbine valve testing. Power was | |||
restored to 100 percent the following day, and remained there for the rest of the inspection period. | |||
Nine Mile Point Unit 2 began the inspection period at full RTP. On July 14, power was reduced to | |||
50 percent due to loss of two high pressure feedwater heaters (FWHs), which resulted from an | |||
electrical transient due to an equipment failure. The FWHs were subsequently returned to | |||
service, and power was restored to 100 percent t he next day. On September 4, an increase in drywell airborne radioactive particulate activity, along with indication of a slowly degrading pump seal for the 'B' RRP and an apparent rapid increase in drywell unidentified leakage, prompted operators to perform a rapid power reduction to 93 percent. It was later determined that drywell | |||
leakage was actually unchanged and stable, as were 'B' RRP seal parameters. Power was | |||
restored to full RTP later that day. On September 18, power was reduced to 86 percent due to a problem with the main transformer cooling system. The problem was resolved and power was | |||
restored to full RTP later that day. Unit 2 continued to operate at full RTP for the remainder of the | |||
inspection period. | |||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01 - One sample) | |||
====a. Inspection Scope==== | |||
On July 24, 2008, the inspectors reviewed NMPNS's actions in response to a severe | |||
electrical storm in the vicinity of the station. During this storm, Unit 1 experienced a | |||
momentary loss of one of the two 115 kilovolt (kV) offsite power lines (line 1) due to a | |||
lightning strike. Offsite power continued to be supplied to both vital switchboards from | |||
offsite line 4, so this event did not result in an automatic start of the associated emergency | |||
diesel generator (EDG). The affected breaker, onsite supply breaker R-10, automatically | |||
reclosed as designed after approximately 5 seconds. The event did not have any | |||
significant effect on plant operations. The inspectors verified that operators implemented | |||
actions specified in the associated procedure to reduce the impact that the adverse | |||
weather had on the site. The inspectors also verified that the NMPNS procedures addressed measures to monitor and maintain availability and reliability of the other offsite alternating current (AC) power system and t he onsite alternate AC power system during adverse weather conditions. | |||
====b. Findings==== | |||
6 No findings of significance were identified. | |||
{{a|1R04}} | {{a|1R04}} | ||
==1R04 Equipment Alignment | ==1R04 Equipment Alignment== | ||
===.1 Partial System Walkdown (71111.04 - Four samples)=== | |||
====a. Inspection Scope==== | |||
The inspectors performed partial system walkdowns to verify risk-significant systems were | |||
properly aligned for operation. The inspectors verified the operability and alignment of | |||
these risk-significant systems while their r edundant trains or systems were inoperable or | |||
out of service for maintenance. The inspec tors compared system lineups to system operating procedures, system drawings, and the applicable chapters in the updated final | |||
safety analysis report (UFSAR). The inspectors verified the operability of critical system | |||
components by observing component material condition during the system walkdown. | |||
The inspectors performed partial walkdowns of the following systems: | |||
* Unit 1 core spray system 111 while core spray system 112 was inoperable for in-service testing; | |||
* Unit 1 core spray system 12 while the 112 core spray topping pump was inoperable and unavailable for maintenance; | |||
* Unit 2 125 volt direct current (DC) electrical system, Divisions 1 and 2, due to high safety significance; and | |||
* Unit 2 high pressure core spray (HPCS) system while the reactor core isolation cooling (RCIC) system was inoperable for maintenance. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
===.2 Complete System Walkdown (71111.04S - One sample)=== | |||
====a. Inspection Scope==== | |||
The inspectors performed a complete walkdown of the Unit 1 emergency service water (ESW) system to identify discrepancies between the existing equipment configuration and | |||
that specified in the design documents. During the walkdown, system drawings and | |||
operating procedures were used to determine the proper equipment alignment and | |||
operational status. The inspectors reviewed the open maintenance work orders (WOs) | |||
that could affect the ability of the system to perform its functions. Documentation | |||
associated with temporary modifications, operator workarounds, and items tracked by | |||
plant engineering were also reviewed to assess their collective impact on system | |||
operation. In addition, the inspectors reviewed the condition report (CR) database to | |||
verify that equipment alignment problems were being identified and appropriately | |||
resolved. | |||
====b. Findings==== | |||
7 No findings of significance were identified. | |||
{{a|1R05}} | {{a|1R05}} | ||
==1R05 Fire Protection............... | ==1R05 Fire Protection== | ||
. | |||
===.1 Quarterly Inspection (71111.05Q - Six samples)=== | |||
====a. Inspection Scope==== | |||
The inspectors toured areas important to reactor safety at NMPNS to evaluate the | |||
station's control of transient combustibles and ignition sources, and to examine the | |||
material condition, operational status, and operational lineup of fire protection systems | |||
including detection, suppression, and fire barriers. The areas inspected included: | |||
* Unit 1 reactor building (RB) 261 foot elevation; | |||
* Unit 1 RB 281 foot elevation; | |||
* Unit 1 emergency cooling system steam isol ation valve room, RB 298 foot elevation; | |||
* Unit 2 RB 261 foot elevation; | |||
* Unit 2 RB 289 foot elevation; and | |||
* Unit 2 RB 353 foot elevation. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
===.2 Annual Inspection (71111.05A - One sample)=== | |||
====a. Inspection Scope==== | |||
The inspectors completed one annual fire drill observation inspection sample. The | |||
inspectors observed a fire brigade drill on September 17, 2008, in the Unit 1 turbine | |||
building. The inspectors observed brigade performance during the drill to evaluate | |||
donning and use of protective equipment and self-contained breathing apparatus, fire | |||
brigade leader command and control, fire brigade response time, communications, and | |||
the use of pre-fire plans. The inspectors attended the post-drill critique and reviewed the | |||
disposition of issues and deficiencies identified during the drill. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
{{a|1R06}} | |||
==1R06 Flood Protection Measures (71111.06 - One sample)== | |||
====a. Inspection Scope==== | |||
The inspectors completed one internal flooding sample. The inspectors reviewed the | |||
individual plant examination and UFSAR for Unit 1 concerning internal flooding events and | |||
completed walkdowns of one area in which flooding could have a significant impact on | |||
risk. The RB torus room and the RB northwest corner room were reviewed. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
{{a|1R07}} | {{a|1R07}} | ||
==1R07 Heat Sink Performance .. | ==1R07 Heat Sink Performance (71111.07A - One sample)== | ||
. | |||
====a. Inspection Scope==== | |||
The inspectors reviewed maintenance records for Unit 1 102 EDG cooling water heat | |||
exchangers 79-03 and 79-04, performed in acco rdance with N1-MPM-079-412, "Diesel Generator Cooling Water Heat Exchanger and Temperature Control Valve Maintenance." | |||
The inspectors reviewed EDG performance data to verify that heat exchanger operation | |||
was consistent with the design basis. The inspectors interviewed the system engineer to | |||
verify overall condition of the heat exchangers. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
{{a|1R11}} | {{a|1R11}} | ||
==1R11 Licensed Operator Requalification Program . | ==1R11 Licensed Operator Requalification Program (71111.11Q - Two samples)== | ||
====a. Inspection Scope==== | |||
The inspectors evaluated two simulator scenarios in the licensed operator requalification | |||
training (LORT) program. The inspectors assessed the clarity and effectiveness of | |||
communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operation, and the oversight and direction provided by | |||
the shift manager. During the scenario, the inspectors also compared simulator | |||
performance with actual plant performance in the control room. The following scenarios | |||
were observed: | |||
* On August 26, 2008, the inspectors observed Unit 1 LORT to assess operator and instructor performance during a scenario involving a main generator hydrogen seal oil pump failure, a grid transient that resulted in a loss of offsite 115 kV power with failure | |||
of the 103 EDG to start, a loss of coolant accident, and failure of the reactor vessel | |||
fuel zone water level indicator. The inspectors evaluated the performance of risk | |||
significant operator actions including the use of special operating procedures (SOPs) | |||
and emergency operating procedures (EOPs). | |||
9 | |||
* On 5 September, 2008, the inspectors observed Unit 2 LORT to assess operator and instructor performance during a scenario involving a loss of drywell cooling, a loss of normal power to the Division 1 and 3 electrical busses, high motor temperature on one | |||
of the operating reactor feedwater pumps that led to loss of the pump, and a loss of | |||
coolant accident in the drywell along with failure of all reactor pressure vessel (RPV) | |||
level indication, requiring RPV flooding. The inspectors evaluated the performance of | |||
risk significant operator actions including the use of SOPs and EOPs. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
{{a|1R12}} | {{a|1R12}} | ||
==1R12 Maintenance Effectiveness .. | ==1R12 Maintenance Effectiveness (71111.12Q - Three samples)== | ||
. | |||
====a. Inspection Scope==== | |||
The inspectors reviewed performance-based problems and the performance and condition | |||
history of selected systems to assess the effectiveness of the maintenance program. The | |||
inspectors reviewed the systems to ensure that the station's review focused on proper | |||
maintenance rule scoping in accordance with 10 CFR Part 50.65, characterization of | |||
reliability issues, tracking system and component unavailability, and 10 CFR Part 50.65 (a)(1) and (a)(2) classification. In addition, the inspectors reviewed the site's ability to | |||
identify and address common cause failures and to trend key parameters. The following | |||
four maintenance rule inspection samples were reviewed: | |||
* Unit 1 125 volt DC system based on multiple uninterruptible power supply (UPS)equipment issues; | |||
* Unit 2 control building heating, ventilation, and air conditioning (HVAC) system based on equipment problems that developed following implementation of a modification; and | |||
* Unit 2 reactor recirculation system based on recirculation pump seal leakage issues. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
{{a|1R13}} | {{a|1R13}} | ||
==1R13 Maintenance Risk Assessments and Emergent Work Control . | ==1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - Six samples)== | ||
====a. Inspection Scope==== | |||
== | The inspectors evaluated the effectiveness of the maintenance risk assessments required | ||
by 10 CFR Part 50.65 (a)(4). The inspectors reviewed equipment logs, work schedules, and performed plant tours to verify that actual plant configuration matched the assessed | |||
configuration. Additionally, the inspectors verified that risk management actions for both | |||
planned and emergent work were consistent with those described in station procedures. | |||
The inspectors reviewed risk assessments for the activities listed below. | |||
Unit 1 10 | |||
* Week of July 14, 2008, that included a rebuild of 112 core spray topping pump, 13 turbine building closed loop cooling system heat exchanger cleaning, and emergent | |||
maintenance to troubleshoot a trip of the 13 instrument air (IA) compressor, combined | |||
within a scheduled maintenance period. | |||
* Week of July 21, 2008, that included 112 containment spray raw water system maintenance and quarterly surveillance, 102 EDG monthly surveillance, and emergent issues with reactor protection system UPS 162B that resulted in a half scram signal, and loss of flow monitoring capability for the electromatic relief valves and safety | |||
valves due to a failed power supply. | |||
* Week of August 18, 2008, that included maintenance on the 13 RRP motor-generator, a power reduction to 85 percent for recovery of 13 RRP, and emergent maintenance to | |||
replace the 103 EDG raw water pump due to low discharge pressure. | |||
Unit 2 | |||
* Week of July 14, 2008, that included Division 1 EDG monthly surveillance, residual heat removal (RHR) 'A' quarterly surveillance, replacement of unannealed red brass | |||
piping in the IA system, and emergent maintenance to troubleshoot a level control | |||
problem with the 2B low pressure FWH, and troubleshooting activities associated with | |||
a radioactive waste sump pump that resulted in multiple plant equipment issues and | |||
required a power reduction to 50 percent. | |||
* Week of July 21, 2008, that included HPCS system maintenance and quarterly surveillance, a 24 hour run of the Division 3 EDG for a two year surveillance, and | |||
emergent maintenance to troubleshoot Division 3 EDG voltage oscillations, a level control problem with the 2B low pressure FWH, and a leak from the low pressure core spray pressure maintenance (keepfill) pump mechanical seal water supply. | |||
* Week of August 4, 2008, that included inspection of the 'B' IA dryer, maintenance on the 'C' IA compressor, weld repair of the 'C' IA receiver, a three day maintenance | |||
period on the RCIC system, and RCIC quarterly surveillance. | |||
====b. Findings==== | |||
=====Introduction.===== | |||
An NRC-identified Green NCV of 10 CFR 50.65(a)(4) was identified for inaccurate risk assessments completed for August 5 and 6, 2008. Specifically, the | |||
unavailable reactor core isolation cooling (RCIC) system was not properly incorporated into the risk assessment. | |||
=====Description.===== | |||
During the week of August 4, 2008, the RCIC system was made inoperable and unavailable on several occasions for planned maintenance activities. When the | |||
inspectors reviewed NMPNS's daily risk assessment on August 6, they noted that RCIC | |||
would be inoperable and unavailable and that the value for daily CDF risk was indicated to | |||
be "Low." The inspectors questioned this, based on previous experience when RCIC | |||
having been unavailable had caused the daily CDF risk to be "Medium." On August 8, 11 NMPNS determined that the daily CDF risk should have been "Medium" while RCIC was | |||
inoperable and unavailable. Prior to this determination, RCIC had been inoperable and | |||
unavailable on two occasions during the week, with a total unavailability time of | |||
approximately 30 hours (hrs). | |||
The cause of the incorrect risk assessment was determined to be that a typographical | |||
error had been made on June 30, 2008, while entering a change to the risk monitor | |||
computer software. This resulted in an error in the coding used to map RCIC | |||
unavailability to risk importance in the Unit 2 PRA model, incorrectly giving it a zero risk | |||
importance. As corrective actions, the modeling of RCIC was corrected and a verification of all mapping codes used in the risk monitor was performed. This issue was entered into the corrective action program (CAP) as CR 2008-6363. | |||
. | |||
The performance deficiency associated with this event was that inaccurate information | |||
was entered in the risk monitor software resulting in an inadequate risk assessment being | |||
used while the RCIC system was inoperable and unavailable during the August 4, 2008 | |||
work week. | |||
== | =====Analysis.===== | ||
The finding was greater than minor because it was similar to IMC 0612, Appendix E, example 7.e, in that the risk assessment for RCIC system maintenance was | |||
= | |||
. | |||
== | |||
inadequate (i.e., it underestimated the risk because of personnel error) because relevant | |||
information provided to the risk assessment tool was inaccurate. As a result, the overall | |||
elevated plant risk, when correctly assessed, put the plant into a higher licensee- | elevated plant risk, when correctly assessed, put the plant into a higher licensee- | ||
established risk category. Per IMC 0609, Attachment 4, Phase 1, "Initial Screening and | |||
Characterization of Findings," the finding was evaluated in accordance with IMC 0609, | established risk category. Per IMC 0609, Attachment 4, Phase 1, "Initial Screening and | ||
Appendix K, "Maintenance Risk Assessment and Risk Management Significance | |||
Determination Process." The baseline (zero-maintenance) core damage frequency was | Characterization of Findings," the finding was evaluated in accordance with IMC 0609, Appendix K, "Maintenance Risk Assessment and Risk Management Significance | ||
1.35E-5/year (yr) and the actual core damage frequency (with | |||
Determination Process." The baseline (zero-maintenance) core damage frequency was | |||
1.35E-5/year (yr) and the actual core damage frequency (with RCIC unavailable) was | |||
5.10E-5/yr. Therefore, the actual incremental core damage frequency was (5.10 - 1.35)E- | 5.10E-5/yr. Therefore, the actual incremental core damage frequency was (5.10 - 1.35)E- | ||
5/yr = 3.75E-5/yr, and the actual incremental core damage probability ( | |||
performed, the value was essentially the zero-maintenance core damage frequency; that | 5/yr = 3.75E-5/yr, and the actual incremental core damage probability (ICDP actual) was (3.75E-5/yr x 30 hrs) / 8760 hrs/yr = 1.28E-7. Although a risk assessment had been | ||
is, it was evaluated the same as if a risk assessment had not been performed. Therefore, | |||
the incremental core damage probability deficit (ICDPD) was equal to | performed, the value was essentially the zero-maintenance core damage frequency; that | ||
ICDPD was less than 1E-6, the finding was determined to be of very low safety | is, it was evaluated the same as if a risk assessment had not been performed. Therefore, the incremental core damage probability deficit (ICDPD) was equal to ICDP actual. Since ICDPD was less than 1E-6, the finding was determined to be of very low safety | ||
significance (Green). The finding had a cross-cutting aspect in the area of human performance because | |||
significance (Green). | |||
per | The finding had a cross-cutting aspect in the area of human performance because | ||
CFR 50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear power plants," subsection (a)(4) states, in part, "Before performing | NMPNS did not appropriately plan work activities by incorporating valid risk insights (H.3.a | ||
maintenance activities . . . the licensee shall assess and manage the increase in risk that | |||
per IMC 0305). | |||
=====Enforcement.===== | |||
10 CFR 50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear power plants," subsection (a)(4) states, in part, "Before performing | |||
maintenance activities . . . the licensee shall assess and manage the increase in risk that | |||
may result from the proposed maintenance activities. The scope of the | may result from the proposed maintenance activities. The scope of the | ||
assessment may be limited to structures, | assessment may be limited to structures, sy stems, and components that a risk-informed evaluation process has shown to be significant to public health and safety." The NMPNS 12 Maintenance Rule Manual classifies the Unit 2 RCIC system as a high safety significant system. Contrary to the above, on August 8, 2008, it was identified that NMPNS had not correctly | ||
assessed the risk associated with maintenance activities on August 5 and August 6 that | |||
had made the Unit 2 RCIC system inoperable and unavailable, in that the daily CDF risk | |||
system. Contrary to the above, on August 8, 2008, it was identified that | |||
had been determined to be "Low" when the actual value was "Medium." Because this | |||
assessed the risk associated with maintenance activities on August 5 and August 6 that | violation is of very low safety significance and was entered into the CAP as CR 2008- | ||
had made the Unit | |||
6363, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000410/2008004-01, Incorrect Risk Assessment for RCIC Unavailability) | |||
CDF risk | |||
had been determined to be "Low" when the actual value was "Medium." Because this | {{a|1R15}} | ||
violation is of very low safety significance and was entered into the | ==1R15 Operability Evaluations (71111.15 - Seven samples)== | ||
CR 2008- | ====a. Inspection Scope==== | ||
6363, this violation is being treated as an | The inspectors evaluated the acceptability of operability evaluations, the use and control | ||
of compensatory measures, and compliance with technical specifications (TSs.) The | |||
evaluations were reviewed using criteria specified in NRC Regulatory Issue Summary | |||
of compensatory measures, and compliance with technical specifications (TSs.) The | |||
evaluations were reviewed using criteria specified in NRC Regulatory Issue Summary | |||
2005-20, "Revision to Guidance Formerly Contained in NRC Generic Letter 91-18, | 2005-20, "Revision to Guidance Formerly Contained in NRC Generic Letter 91-18, | ||
'Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution | 'Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution | ||
of Degraded and Nonconforming Conditions and on Operability'," and Inspection Manual | |||
Part 9900, "Operability Determinations and Functionality Assessments for Resolution of | of Degraded and Nonconforming Conditions and on Operability'," and Inspection Manual | ||
Degraded or Nonconforming Conditions Adverse to Quality or Safety." The inspectors' | |||
review included verification that the operability determinations were made as specified by | Part 9900, "Operability Determinations and Functionality Assessments for Resolution of | ||
Procedure | |||
Degraded or Nonconforming Conditions Adverse to Quality or Safety." The inspectors' | |||
OP-1.01-1002, "Conduct of Operability Determinations / Functionality | |||
Assessments." The technical adequacy of the determinations was reviewed and compared to the | review included verification that the operability determinations were made as specified by | ||
UFSAR, and associated design basis documents (DBDs). The following evaluations were reviewed: | Procedure CNG-OP-1.01-1002, "Conduct of Operability Determinations / Functionality | ||
Assessments." The technical adequacy of the determinations was reviewed and compared to the TSs, UFSAR, and associated design basis documents (DBDs). | |||
The following evaluations were reviewed: | |||
* CR 2008-5852 concerning the operability of the Unit 1 drywell equipment drain tank input to the drywell leak detection system, in light of anomalous tank level and leak rate indications; | |||
* CR 2008-6536 concerning degraded flow from the Unit 1 EDG 103 raw water pump, identified during its quarterly surveillance; | |||
* CR 2008-6643 concerning water and sediment in Unit 1 EDG fuel oil storage tank bottom samples; | |||
* CR 2008-5841 concerning degraded performance of one of the Unit 2 'A' RHR pump room unit coolers; | |||
* CR 2008-5439 concerning operability of the Unit 2 Division 2 EDG in the emergency mode with a failed overspeed butterfly valve limit switch that had caused the EDG to shut down while operating in the test mode; | |||
* CR 2008-5885 concerning the effect of increased Unit 2 suppression pool leakage on emergency core cooling system pump operability; and | |||
* CR 2008-6647 concerning low peak firing pressure on one cylinder for the Unit 2 Division 3 EDG. | |||
CR 2008-6647 concerning low peak firing pressure on one cylinder for the Unit 2 Division 3 EDG. | ====b. Findings==== | ||
b. Findings | No findings of significance were identified. | ||
{{a|1R18}} | |||
No findings of significance were identified. 1R18 Plant Modifications (71111.18 - Four samples) | ==1R18 Plant Modifications (71111.18 - Four samples)== | ||
.1 Temporary Modifications | |||
a. Inspection Scope | ===.1 Temporary Modifications=== | ||
====a. Inspection Scope==== | |||
The inspectors reviewed a Unit 2 temporary modification to raise the 'D' service water | |||
pump outboard bearing temperature setpoint from 130 degrees Fahrenheit (F) to 150 F. | pump outboard bearing temperature setpoint from 130 degrees Fahrenheit (F) to 150 F. | ||
The inspectors reviewed a Unit 2 temporary modification that installed temporary power to | The setpoint was raised to allow for new packing run-in on the pump. The inspectors | ||
the B-phase main transformer cooling pumps and fans from the installed spare 'D' main | |||
transformer. The inspectors reviewed the at-risk activity work package, interviewed the system engineer, and reviewed the 10 CFR Part 50.59 screening against the system design bases documentation to verify that the modification did not affect system | reviewed the 10 CFR Part 50.59 screening against the system design bases | ||
operability. The inspectors also reviewed the WO that installed and removed the | |||
temporary power and walked down the equipment after work completion to verify that the | documentation to verify that the modification did not affect system operability. The | ||
inspectors reviewed the vendor manual to verify that increased temperature would not | |||
affect the pump's reliability. | |||
The inspectors reviewed a Unit 2 temporary modification that installed temporary power to | |||
the B-phase main transformer cooling pumps and fans from the installed spare 'D' main | |||
transformer. The inspectors reviewed the at-risk activity work package, interviewed the system engineer, and reviewed the 10 CFR Part 50.59 screening against the system design bases documentation to verify that the modification did not affect system | |||
operability. The inspectors also reviewed the WO that installed and removed the | |||
temporary power and walked down the equipment after work completion to verify that the | |||
equipment had been returned to its original configuration. | equipment had been returned to its original configuration. | ||
.2 Permanent Modifications | ====b. Findings==== | ||
a. Inspection Scope | No findings of significance were identified. | ||
Effluent Monitoring System Replacement." | |||
assessed the adequacy of the modification package and procedural changes, verified that | ===.2 Permanent Modifications=== | ||
applicable design and licensing basis requirements were met, and verified that design | |||
margins were not degraded by the modification. | ====a. Inspection Scope==== | ||
The inspectors reviewed Unit 2 design change package (DCP) N2-99-032, "Gaseous | |||
Effluent Monitoring System Replacement." | |||
The purpose of this modification was to replace an aging system for which system reliability had been degrading. The inspectors | |||
assessed the adequacy of the modification package and procedural changes, verified that | |||
applicable design and licensing basis requirements were met, and verified that design | |||
margins were not degraded by the modification. | |||
The inspectors reviewed Unit 1 DCP N1-08-013, "Replace Control Rod Drive (CRD) | |||
Timing Recorders at NMP1." The purpose of this modification was to improve the process | |||
by which data is acquired and analyzed for all control rod movement. The inspectors | |||
assessed the adequacy of the modification package and 10 CFR Part 50.59 screening, verified that applicable design and licensing basis requirements were met, and verified that design margins were not degraded by the modification. The inspectors interviewed | |||
engineers involved with the project, walked down the system, and reviewed the post-14 maintenance test (PMT) results to verify proper installation and the test acceptance criteria | |||
had been met. The inspectors also reviewed the affected procedures and drawings to | |||
verify that affected documents were being updated. | verify that affected documents were being updated. | ||
b. Findings | |||
No findings of significance were identified. 1R19 Post Maintenance Testing (71111.19 - Seven samples) | ====b. Findings==== | ||
a. Inspection Scope | No findings of significance were identified. | ||
procedure to verify that the procedure adequately tested the safety functions that may | {{a|1R19}} | ||
have been affected by the maintenance activity, that the acceptance criteria in the | ==1R19 Post Maintenance Testing (71111.19 - Seven samples)== | ||
procedure were consistent with information in the applicable licensing basis and/or DBDs, | |||
and that the procedure had been properly reviewed and approved. The inspectors also | ====a. Inspection Scope==== | ||
witnessed the test or reviewed test data, to verify that the test results adequately | The inspectors reviewed the PMTs listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test | ||
demonstrated restoration of the affected safety functions. . * Unit 1, | |||
procedure to verify that the procedure adequately tested the safety functions that may | |||
have been affected by the maintenance activity, that the acceptance criteria in the | |||
EPM-UPS-003, "UPS 10 | |||
Year Maintenance," and a 24-hour confidence run. | procedure were consistent with information in the applicable licensing basis and/or DBDs, and that the procedure had been properly reviewed and approved. The inspectors also | ||
witnessed the test or reviewed test data, to verify that the test results adequately | |||
demonstrated restoration of the affected safety functions. | |||
PMT was performed in accordance with N1-ST-Q1C, "Core Spray 112 Pump and Valve | . | ||
Operability Test," and N1-PM-V2, "Pump Curve Validation Test." | * Unit 1, WO 08-11429-00 that replaced capacitors in uninterruptable power supply UPS-162A. The PMT was performed in accordance with N1-EPM-UPS-003, "UPS 10 | ||
Year Maintenance," and a 24-hour confidence run. | |||
* Unit 1, WO 08-13901-00 that replaced the EDG 103 raw water pump. The PMT was performed in accordance with N1-ST-Q25, "EDG Cooling Water Quarterly Test," and N1-PM-V2, "Pump Curve Validation Test." | |||
* Unit 1, WO 08-09002-00 that rebuilt the 112 core spray topping pump. The PMT was performed in accordance with N1-ST-Q1C, "Core Spray 112 Pump and Valve | |||
PMT was performed in accordance with N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability | Operability Test," and N1-PM-V2, "Pump Curve Validation Test." | ||
Test - Division I and II." | * Unit 1, WO 06-20738-00 that performed preventive maintenance on stack off-gas radiation monitor, RAM-112-08A. The PMT was performed in accordance with N1- | ||
ISP-112-001, "Stack Gas Monitor Calibration." | |||
* Unit 2, ACR 08-04217 that performed troubleshooting of the Division 2 EDG overspeed butterfly valve limit switch fa ilure. The PMT was performed in accordance with N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability | |||
Test - Division I and II." | |||
* Unit 2, ACR 08-04603 that performed troubleshooting of the Division 3 EDG voltage regulator motor operated potentiometer. The PMT was performed in accordance with N2-OP-100B, "HPCS Diesel Generator." | |||
* Unit 2, WO 06-13888-00 that rebuilt service water pump 2SWP*P1D. The PMT was 15 performed in accordance with N2-OSP-SWP-@001, "Service Water Pump Curve | |||
Validation Test." | Validation Test." | ||
The following surveillance tests were reviewed: | ====b. Findings==== | ||
No findings of significance were identified. | |||
{{a|1R22}} | |||
==1R22 Surveillance Testing (71111.22 - Eight samples)== | |||
====a. Inspection Scope==== | |||
TSP-HVC-R@001, "Testing and Analysis of Unit 2 Control Room Outdoor Air Special Filter Train System." | The inspectors witnessed performance of and/or reviewed test data for risk-significant | ||
16 Cornerstone: Emergency Preparedness | |||
surveillance tests to assess whether the components and systems tested satisfied design and licensing basis requirements. The inspectors verified that test acceptance criteria | |||
were clear, demonstrated operational readiness and were consistent with the DBDs; that | |||
test instrumentation had current calibrations and the range and accuracy for the | |||
application; and that tests were performed, as written, with applicable prerequisites | |||
satisfied. Upon test completion, the inspectors verified that equipment was returned to the | |||
status specified to perform its safety function. | |||
The following surveillance tests were reviewed: | |||
* N1-ST-Q2, "Control Rod Drive Pumps Flow Rate Test;" | |||
* N1-ST-Q13, "Emergency Service Water Pump Operability Test;" | |||
* N1-ST-M4A, "EDG 102 and PB 102 Operability Test;" | |||
* N1-ST-Q6A, "Containment Spray System Loop 111 Quarterly Operability Test;" | |||
* N2-PM-A006, "B.5.b Pump Annual Flow Rate Test;" | |||
* N2-OSP-ICS-Q@002, "RCIC Pump and Valve Operability Test and System Integrity Test and ASME XI Functional Test;" | |||
* N2-OSP-SWP-Q@001, "Division 1 SW Operability Test;" and | |||
* N2-TSP-HVC-R@001, "Testing and Analysis of Unit 2 Control Room Outdoor Air Special Filter Train System." | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
16 Cornerstone: Emergency Preparedness 1EP2 Alert and Notification System Evaluation (71114.02 - One sample) | |||
====a. Inspection Scope==== | |||
An onsite review was conducted to assess the maintenance and testing of the NMPNS | |||
alert and notification system (ANS), including both the system sirens and tone alert radios. | alert and notification system (ANS), including both the system sirens and tone alert radios. | ||
During this inspection, the inspectors interviewed emergency preparedness (EP) staff | |||
responsible for implementation of the ANS testing and maintenance. The inspectors | During this inspection, the inspectors interviewed emergency preparedness (EP) staff | ||
reviewed | |||
responsible for implementation of the ANS testing and maintenance. The inspectors | |||
reviewed CRs pertaining to the ANS for causes, trends, and NMPNS's corrective actions. | |||
The inspectors further discussed the ANS with the assigned technical specialist, reviewing | The inspectors further discussed the ANS with the assigned technical specialist, reviewing | ||
system performance from June 2006 through June 2008. The inspectors reviewed the | |||
system performance from June 2006 through June 2008. The inspectors reviewed the | |||
ANS procedures and the ANS design report to ensure NMPNS's compliance with those | |||
commitments for system maintenance and testing. Additionally, the inspectors reviewed | commitments for system maintenance and testing. Additionally, the inspectors reviewed | ||
changes to the design report and how these changes were captured. The Planning | |||
Standard, | changes to the design report and how these changes were captured. The Planning | ||
CFR Part 50, Appendix E, were used as reference criteria. b. Findings | Standard, 10 CFR Part 50.47(b)(5), and the related requirements of 10 CFR Part 50, Appendix E, were used as reference criteria. | ||
====b. Findings==== | |||
No findings of significance were identified. | |||
1EP3 Emergency Response Organization Staffing and Augmentation System (71114.03 - One sample) | 1EP3 Emergency Response Organization Staffing and Augmentation System (71114.03 - One sample) | ||
a. Inspection Scope | |||
====a. Inspection Scope==== | |||
The inspectors conducted a review of the NMPNS emergency response organization (ERO) augmentation staffing requirements and the process for notifying and augmenting | |||
(ERO) augmentation staffing requirements and the process for notifying and augmenting | |||
the ERO. This was performed to ensure the readiness of key staff for responding to an | the ERO. This was performed to ensure the readiness of key staff for responding to an | ||
event and to ensure timely facility activation. The inspectors reviewed procedures and | |||
event and to ensure timely facility activation. The inspectors reviewed procedures and | |||
ERO notification system and drills, and reviewed records from | |||
call-in drills. The inspectors interviewed personnel responsible for testing the ERO | CRs associated with the ERO notification system and drills, and reviewed records from | ||
augmentation process, and reviewed the training records for a sampling of ERO to ensure | |||
training and qualifications were up to date. The inspectors reviewed procedures for ERO | call-in drills. The inspectors interviewed personnel responsible for testing the ERO | ||
administration and training, and verified a sampling of ERO participation in exercises and | |||
drills in 2007 and 2008. The Planning Standard, | augmentation process, and reviewed the training records for a sampling of ERO to ensure | ||
CFR Part 50, Appendix E, were used as reference criteria. b. Findings | training and qualifications were up to date. The inspectors reviewed procedures for ERO | ||
administration and training, and verified a sampling of ERO participation in exercises and | |||
drills in 2007 and 2008. The Planning Standard, 10 CFR Part 50.47(b)(2) and related requirements of 10 CFR Part 50, Appendix E, were used as reference criteria. | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - One sample) | 1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - One sample) | ||
a. Inspection Scope | |||
====a. Inspection Scope==== | |||
Prior to this inspection, the NRC had received and acknowledged changes made to the | |||
NMPNS developed these changes in accordance with 10 CFR Part 50.54(q), and determined that the changes did | |||
not result in a decrease in effectiveness of the | NMPNS emergency plan and its implementi ng procedures. NMPNS developed these changes in accordance with 10 CFR Part 50.54(q), and determined that the changes did | ||
not result in a decrease in effectiveness of the NMPNS Site Emergency Plan (the Plan). | |||
CFR Part | NMPNS also determined that the Plan continued to meet the requirements of 10 CFR Part | ||
50.47(b) and Appendix E to 10 CFR Part 50. During this inspection, the inspectors | |||
conducted a review of | 50.47(b) and Appendix E to 10 CFR Part 50. During this inspection, the inspectors | ||
CFR Part 50.54(q) screenings for all the changes made to the emergency action levels (EALs) and all of the changes made to the Plan from | conducted a review of NMPNS | ||
August 2007 through June 2008 that could have potentially resulted in a decrease in effectiveness of the Plan. This review of the | =s 10 CFR Part 50.54(q) screenings for all the changes made to the emergency action levels (EALs) and all of the changes made to the Plan from | ||
NRC approval of the changes and, as such, the changes remain subject to future NRC | August 2007 through June 2008 that could have potentially resulted in a decrease in effectiveness of the Plan. This review of the EALs and Plan changes did not constitute NRC approval of the changes and, as such, the changes remain subject to future NRC | ||
inspection. The requirements in 10 CFR Part 50.54(q) were used as reference criteria. | inspection. The requirements in 10 CFR Part 50.54(q) were used as reference criteria. | ||
b. Findings | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
1EP5 Correction of Emergency Preparedness Weaknesses (71114.05 - One sample) | 1EP5 Correction of Emergency Preparedness Weaknesses (71114.05 - One sample) | ||
a. Inspection Scope | |||
====a. Inspection Scope==== | |||
The inspectors reviewed a sampling of self-assessment procedures and reports to assess | |||
NMPNS=s ability to evaluate their EP performance and programs. The inspectors reviewed a sampling of CRs from January 2007 through June 2008 initiated by NMPNS | |||
concerning drills, self-assessments, and audits. Additionally, the inspectors reviewed: | |||
concerning drills, self-assessments, and audits. Additionally, the inspectors reviewed: | |||
CFR Part | EP Oversight Board meeting minutes; Qualit y and Performance Assurance reports; event reports for the September 2007 Alert and the May 2008 Unusual Event declarations at | ||
50.47(b)(14), and the related requirements of 10 CFR Part 50, Appendix E, were used as | |||
NMPNS; and the 2007 50.54(t) audit report. The Planning Standard, 10 CFR Part | |||
50.47(b)(14), and the related requirements of 10 CFR Part 50, Appendix E, were used as | |||
reference criteria. | reference criteria. | ||
b. Findings | |||
====b. Findings==== | |||
No findings of significance were identified. | |||
1EP6 Drill Evaluation (71114.06 - One sample) | 1EP6 Drill Evaluation (71114.06 - One sample) | ||
a. Inspection Scope | |||
the Unit 2 evaluated | ====a. Inspection Scope==== | ||
The inspectors observed control room operator emergency plan response actions during | |||
emergency classification declarations and notifications were completed in accordance with | the Unit 2 evaluated LORT scenario on September 5, 2008. The inspectors verified that | ||
CFR Part 50 Appendix E, and the emergency implementing | emergency classification declarations and notifications were completed in accordance with 18 10 CFR Part 50.72, 10 CFR Part 50 Appendix E, and the emergency implementing | ||
procedures. | procedures. | ||
====b. Findings==== | |||
No findings of significance were identified. | |||
==RADIATION SAFETY== | |||
===Cornerstone:=== | |||
Occupational Radiation Safety 2OS1 Access Control to Radiologically Significant Areas (71121.01 - Six samples) | |||
====a. Inspection Scope==== | |||
The inspectors reviewed radiation work permits for airborne radioactivity areas with the potential for individual worker internal exposures of greater than 50 millirem (mrem) | |||
committed effective dose equivalent (20 derived air concentration (DAC)-hours). For | |||
these selected airborne radioactive material areas, the inspectors verified barrier integrity | |||
and engineering controls performance (e.g., high efficiency particulate air ventilation | |||
system operation). | |||
The inspectors evaluated | The inspectors reviewed and assessed the adequacy of NMPNS's internal dose | ||
assessment for any actual internal exposur e greater than 50 mrem committed effective dose equivalent. | |||
TS 6.12. | The inspectors examined NMPNS's physical and programmatic controls for highly | ||
activated or contaminated materials (non-fuel) stored within the spent fuel pools. | |||
The inspectors discussed with the acting radiation protection manager high dose rate-high | |||
radiation area, and very high radiation area controls and procedures. The inspectors | |||
focused on any procedural changes since the last inspection. The inspectors verified that | |||
any changes to NMPNS's procedures did not substantially reduce the effectiveness and level of worker protection. | |||
The inspectors discussed with health physics supervisors the controls in place for special | |||
areas that have the potential to become very high radiation areas during certain plant | |||
operations. The inspectors determined if these plant operations required communication | |||
beforehand with the health physics group, so as to allow corresponding timely actions to | |||
properly post and control the radiation hazards. | |||
The inspectors verified adequate posting and locking of all entrances to high dose rate- | |||
high radiation areas, and very high radiation areas. | |||
The inspectors evaluated NMPNS's performance against the requirements contained in 10 CFR Part 20, Unit 1 TS 6.7, and Unit 2 TS 6.12. | |||
====b. Findings==== | |||
No findings of significance were identified. | No findings of significance were identified. | ||
The inspectors obtained from | 2OS2 ALARA Planning and Controls (71121.02 - Four samples) | ||
====a. Inspection Scope==== | |||
selected the two work activities of highest exposure significance. | The inspectors reviewed the results of the Spring 2008 Unit 2 refueling outage (2RFO11), | ||
including the causes of any radiologically significant work (greater than five person-rem | |||
collective exposure) which exceeded its dose estimate. | |||
The inspectors obtained from NMPNS a list of wo rk activities ranked by actual/estimated exposure that are in progress or that have been completed during the last outage and | |||
selected the two work activities of highest exposure significance. | |||
The inspectors reviewed the as low as r easonably achievable (ALARA) work activity evaluations, exposure estimates, and exposure mitigation requirements. The inspectors | |||
determined if NMPNS had established procedures, engineering and work controls, based on sound radiation protection principles to achieve occupational exposures that were ALARA. The inspectors determined if NMPNS had reasonably grouped the radiological | |||
work into work activities, based on historic al precedence, industry norms, and/or special circumstances. | |||
The inspectors compared the results achieved (dose rate reductions, person-rem used) | |||
with the intended dose established in NMPNS's ALARA planning for these work activities. | |||
The inspectors reviewed the assumptions and basis for the current annual collective | |||
exposure estimate. The inspectors reviewed applicable procedures to determine the | |||
with the intended dose established in | |||
methodology for estimating work activity-specific exposures and the intended dose outcome. The inspectors evaluated both dose rate and man-hour estimates for | |||
ALARA planning for these work activities. | |||
reasonable accuracy. | |||
The inspectors reviewed NMPNS's method for adjusting exposure estimates, or re- | |||
planning work, when unexpected changes in scope or emergent work are encountered. | planning work, when unexpected changes in scope or emergent work are encountered. | ||
The inspectors determined if adjustments to estimated exposure (intended dose) were | |||
based on sound radiation protection and | The inspectors determined if adjustments to estimated exposure (intended dose) were | ||
based on sound radiation protection and ALARA principles or just adjusted to account for | |||
failures to control the work. | failures to control the work. | ||
20 | The inspectors evaluated NMPNS's performance against the requirements contained in 10 CFR Part 20.1101. | ||
====b. Findings==== | |||
No findings of significance were identified. | |||
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - One sample) | 2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - One sample) | ||
The inspectors | ====a. Inspection Scope==== | ||
The inspectors reviewed the plant UFSAR to identify applicable radiation monitors | |||
associated with transient high and very high radiation areas including those used in | |||
CFR Part 20.1703 and 10 CFR Part 20.1704. | |||
b. Findings | remote emergency assessment. | ||
No findings of significance were identified. | |||
The inspectors evaluated NMPNS's performance against the requirements contained in 10 | |||
CFR Part 20.1501, 10 CFR Part 20.1703 and 10 CFR Part 20.1704. | |||
====b. Findings==== | |||
PI definition | No findings of significance were identified. | ||
guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment | |||
Performance Indicator Guideline," Revision 5, was used to verify the basis in reporting for | ==OTHER ACTIVITIES== | ||
each data element. | {{a|4OA1}} | ||
==4OA1 Performance Indicator Verification (71151 - Seven samples)== | |||
====a. Inspection Scope==== | |||
The inspectors sampled NMPNS submittals fo r the performance indicators (PIs) listed below. To verify the accuracy of the PI data reported during that period, the PI definition | |||
guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment | |||
Performance Indicator Guideline," Revision 5, was used to verify the basis in reporting for | |||
each data element. | |||
===Cornerstone:=== | |||
Initiating Events | |||
The inspectors reviewed licensee event reports (LERs) and operator logs to determine | |||
whether NMPNS accurately reported the number of unplanned power changes greater | |||
than 20 percent at Unit 1 and Unit 2 from October 2007 to June 2008. | |||
* Unit 1 unplanned power changes per 7000 critical hours | |||
* Unit 2 unplanned power changes per 7000 critical hours | |||
===Cornerstone:=== | |||
Mitigating Systems | |||
Unit 1 and Unit 2 LERs issued between the end of the third quarter 2007 and the end of | |||
the second quarter 2008 were reviewed for safety system functional failures. | |||
* Unit 1 safety system functional failures | |||
* Unit 2 safety system functional failures 21 Cornerstone: Emergency Preparedness The inspectors reviewed data for the EP PIs which are: drill and exercise performance; | |||
ERO Drill Participation; and ANS Reliability. The inspectors reviewed the PI data, its | |||
supporting documentation, and the information NMPNS reported for the third and fourth | |||
quarters of 2007, and the first and second quarters of 2008, to verify the accuracy of the | |||
reported data. The acceptance criteria used for the review were 10 CFR Part 50.9 and | |||
NEI 99-02. | NEI 99-02. | ||
Additionally, the inspectors performed | |||
Additionally, the inspectors performed NRC Temporary Instruction (TI) 2515/175, ensured the completeness of NMPNS's completed Attachment 1 from the TI, and forwarded that | |||
data to NRC Headquarters. | |||
TI, and forwarded that | |||
data to | ====b. Findings==== | ||
No findings of significance were identified. | |||
{{a|4OA2}} | |||
a. Inspection Scope | ==4OA2 Identification and Resolution of Problems (71152 - Two samples)== | ||
and in order to help identify repetitive equipment failures or specific human performance | |||
issues for follow-up, the inspectors performed a daily screening of items entered into | ===.1 Review of Items Entered into the CAP=== | ||
CAP. In accordance with the baseline inspection procedures, the inspectors | ====a. Inspection Scope==== | ||
also identified selected CAP items across | As specified by Inspection Procedure 71152, "Identification and Resolution of Problems," | ||
the threshold for problem identification, the adequacy of the cause analyses, extent of | |||
condition review, operability determinations, and the timeliness of the specified corrective | and in order to help identify repetitive equipment failures or specific human performance | ||
issues for follow-up, the inspectors performed a daily screening of items entered into | |||
NMPNS's CAP. In accordance with the baseline inspection procedures, the inspectors | |||
also identified selected CAP items across t he initiating events, mitigating systems, and barrier integrity cornerstones for additional follow-up and review. The inspectors assessed | |||
the threshold for problem identification, the adequacy of the cause analyses, extent of | |||
condition review, operability determinations, and the timeliness of the specified corrective | |||
actions. | actions. | ||
The inspectors selected the FWH issue for review because it resulted in an unplanned | ====b. Findings==== | ||
reactivity change and power reduction, caused significant water-hammer in the system, | No findings of significance were identified. | ||
and challenged plant operators. The inspectors reviewed | |||
===.2 Annual Sample - Review of Corrective Actions for Unit 1 Feedwater Heater Issues=== | |||
troubleshooting results, root cause evaluation, extent of condition review, and short-term and long-term corrective actions. The inspectors conducted a walkdown of accessible portions of the system, and reviewed the material condition of the LCVs, design control | ====a. Inspection Scope==== | ||
measures, and configuration control. The inspectors also interviewed plant personnel and | This inspection focused on NMPNS's problem identification, evaluation, and resolution of | ||
reviewed procedures, related industry operating experience (OE), and the vendor manual | |||
for the | a Unit 1 level control valve (LCV)-26-09 actuator o-ring issue associated with the 122 | ||
FWH. On September 15, 2007, the 122 FWH tripped on high-high level when LCV-26-09 | |||
failed in the closed position and caused a cascading affect that backed up the water flow | |||
NMPNS operated and maintained the FWH system as required. | to the other FWHs in the heater string. The 121 through 124 FWHs tripped due to high- | ||
high level within 30 minutes, and the last FWH in the heater string (125) tripped several 22 hours later. This caused operators to reduce reactor power to less than 80 percent and | |||
produced significant water-hammer in the FWH system piping. Following this event, operators initiated a condition report (CR 2007-5475) to resolve the issue. NMPNS | |||
performed corrective maintenance on the valve actuator o-ring and repaired damaged | |||
piping and supports on the 12 heater string prior to returning the system to service. | |||
The inspectors selected the FWH issue for review because it resulted in an unplanned | |||
reactivity change and power reduction, caused significant water-hammer in the system, and challenged plant operators. The inspectors reviewed NMPNS's associated | |||
troubleshooting results, root cause evaluation, extent of condition review, and short-term and long-term corrective actions. The inspectors conducted a walkdown of accessible portions of the system, and reviewed the material condition of the LCVs, design control | |||
measures, and configuration control. The inspectors also interviewed plant personnel and | |||
reviewed procedures, related industry operating experience (OE), and the vendor manual | |||
for the FWH LCV actuators. In addition, the inspectors reviewed the NMPNS TS and | |||
UFSAR to ensure that NMPNS operated and maintained the FWH system as required. | |||
b. Assessment and Observations | b. Assessment and Observations | ||
No findings of significance were identified. | |||
No findings of significance were identified. NMPNS used a failure modes and effects | |||
analysis in the root cause evaluation to determine the nature of the LCV malfunction. The | analysis in the root cause evaluation to determine the nature of the LCV malfunction. The | ||
root cause evaluation determined that the lubricant used in the actuator degraded to the | |||
point where it caused the actuator o-rings to harden, thereby allowing air to leak past the | root cause evaluation determined that the lubricant used in the actuator degraded to the | ||
actuating piston. This caused insufficient air pressure to the valve actuator such that it | |||
would not open the | point where it caused the actuator o-rings to harden, thereby allowing air to leak past the | ||
actuating piston. This caused insufficient air pressure to the valve actuator such that it | |||
would not open the LCV on a demand signal. The inspectors determined that NMPNS | |||
performed a thorough review of the issue and implemented appropriate corrective actions. | performed a thorough review of the issue and implemented appropriate corrective actions. | ||
The corrective actions were aligned with the root cause analysis and included procedure | |||
and preventive maintenance revisions, | The corrective actions were aligned with the root cause analysis and included procedure | ||
operating experience program improvements. The inspectors concluded that | |||
and preventive maintenance revisions, implement ing the use of a new lubricant, improved training to operators and engineering personnel on water-hammer mechanisms, and | |||
CAP. The | |||
inspectors also determined that the root cause evaluation and subsequent follow-up | operating experience program improvements. | ||
corrective maintenance were generally sufficient and based on the best available | |||
information, troubleshooting, and relevant industry | The inspectors concluded that NMPNS had taken appropriate action in accordance with station procedures and the CAP. The | ||
NMPNS's assigned | inspectors also determined that the root cause evaluation and subsequent follow-up | ||
corrective actions were adequately tracked, appropriately documented, and completed as | |||
scheduled. | corrective maintenance were generally sufficient and based on the best available | ||
a. Inspection Scope | information, troubleshooting, and relevant industry OE. In general, NMPNS's assigned | ||
corrective actions were adequately tracked, appropriately documented, and completed as | |||
September 19, 2007 inadvertent discharge of | |||
scheduled. | |||
===.3 Annual Sample - Review of Corrective Actions for Inadvertent Carbon Dioxide (CO2)=== | |||
CR 2007-5538). The event occurred during | |||
an installation of wiring in a local fire panel as part of a design change, and resulted in | Discharge | ||
NMPNS's root cause | ====a. Inspection Scope==== | ||
analysis and corrective actions to ensure that appropriate evaluations were performed and | The inspectors reviewed NMPNS's evaluation and corrective actions associated with the | ||
September 19, 2007 inadvertent discharge of CO2 from the fixed CO2 fire suppression system in the Unit 2 HPCS switchgear room (CR 2007-5538). The event occurred during | |||
an installation of wiring in a local fire panel as part of a design change, and resulted in | |||
NMPNS declaring an Alert at Unit 2. The inspectors reviewed NMPNS's root cause | |||
analysis and corrective actions to ensure that appropriate evaluations were performed and 23 corrective actions were specified and prioritized. The inspectors also reviewed the follow- | |||
up actions to verify that the root cause and corrective actions identified were addressed. | up actions to verify that the root cause and corrective actions identified were addressed. | ||
b. Findings & Observations | |||
corrective actions taken associated with the inadvertent CO2 discharge were reasonable | ====b. Findings==== | ||
and adequate. 4OA3 Followup of Events and Notices of Enforcement Discretion (71153 - Three samples) | & Observations No findings of significance were identified. The inspectors determined that, in general, the | ||
.1 (Closed) LER 05000220/2008-001-00, Loss of Offsite Power due to an Equipment Malfunction | |||
failure which caused a loss of 115 kV offsite power line 4 while the remaining 115 kV | corrective actions taken associated with the inadvertent CO2 discharge were reasonable | ||
offsite power line (line 1) was removed from service for planned maintenance. The event | |||
detailed in this | and adequate. | ||
{{a|4OA3}} | |||
05000220/2008003. The inspectors reviewed this LER and no findings of significance | ==4OA3 Followup of Events and Notices of Enforcement Discretion (71153 - Three samples)== | ||
were identified. This LER is closed. | |||
.2 (Closed) | ===.1 (Closed) LER 05000220/2008-001-00 , Loss of Offsite Power due to an Equipment=== | ||
NMPNS discovered that the J10 alarm relays in RB ventilation system | Malfunction On May 13, 2008, a loss of Unit 1 offsite power occurred due to an offsite equipment | ||
unit cooler motor starter circuits did not satisfy the environmental qualification | |||
requirements of 10 CFR 50.49. This discovery came as a result of investigation of the | failure which caused a loss of 115 kV offsite power line 4 while the remaining 115 kV | ||
cause of J10 relay failures during loss of offsite power testing that was performed during | |||
the 2008 refueling outage. J10 relay failures resulted in an NCV as documented in | offsite power line (line 1) was removed from service for planned maintenance. The event | ||
Section 1R22 of Inspection Report 05000410/2008003. The inspectors reviewed this LER | |||
and no additional findings of significance were identified. The failure of the J10 relays to | detailed in this LER was discussed in Section | ||
meet the environmental qualification requirements of 10 CFR 50.49 constitutes a violation | {{a|4OA3}} | ||
of minor significance that is not subject to enforcement action in accordance with Section | ==4OA3 of Inspection Report== | ||
05000220/2008003. The inspectors reviewed this LER and no findings of significance | |||
were identified. This LER is closed. | |||
LER is closed. | ===.2 (Closed) LER 05000410/2008-001-00 , Unqualified Relays Installed Since Original=== | ||
a. Inspection Scope | |||
of extraction steam to the 6B (high pressure) and 5C (low pressure) FWHs. The cause of | Construction Result in an Unanalyzed Condition On April 10, 2008, NMPNS discovered that the J10 alarm relays in RB ventilation system | ||
the event was an unrelated maintenance activity that unexpectedly produced an electrical | |||
transient which affected a number of plant systems. Other consequences of the transient | unit cooler motor starter circuits did not satisfy the environmental qualification | ||
were loss of the 'A' and 'C' heater drain pumps, loss of the 'B' offgas train, loss of normal | |||
requirements of 10 CFR 50.49. This discovery came as a result of investigation of the | |||
RB and start of the standby gas | |||
cause of J10 relay failures during loss of offsite power testing that was performed during | |||
the 2008 refueling outage. J10 relay failures resulted in an NCV as documented in | |||
Section 1R22 of Inspection Report 05000410/2008003. The inspectors reviewed this LER | |||
and no additional findings of significance were identified. The failure of the J10 relays to | |||
meet the environmental qualification requirements of 10 CFR 50.49 constitutes a violation | |||
of minor significance that is not subject to enforcement action in accordance with Section | |||
IV of the NRC Enforcement Policy. NMPNS entered the issues associated with this event into its CAP as CR 2008-2976. This LER is closed. | |||
===.3 Power Reduction due to a Maintenance-Related Electrical Transient=== | |||
====a. Inspection Scope==== | |||
On July 14 at 1:12 p.m., Unit 2 experienced a partial loss of feedwater heating due to loss | |||
of extraction steam to the 6B (high pressure) and 5C (low pressure) FWHs. The cause of | |||
the event was an unrelated maintenance activity that unexpectedly produced an electrical | |||
transient which affected a number of plant systems. Other consequences of the transient | |||
were loss of the 'A' and 'C' heater drain pumps, loss of the 'B' offgas train, loss of normal | |||
RB ventilation which resulted in automatic isolation of the RB and start of the standby gas | |||
treatment system, and isolation of the hydrogen water chemistry system. | treatment system, and isolation of the hydrogen water chemistry system. | ||
N2-SOP-101D, "Rapid Power Reduction," to lower reactor power to 73 percent. After the | 24 Operators responded in accordance with N2-SOP-08, "Unplanned Power Changes," and | ||
cause of the transient was identified, operators commenced recovery of the FWHs. While | |||
attempting to restore the 5C FWH to service, resultant system perturbations caused an | N2-SOP-101D, "Rapid Power Reduction," to lower reactor power to 73 percent. After the | ||
isolation of the 6C | |||
cause of the transient was identified, operators commenced recovery of the FWHs. While | |||
FWHs (6B and 6C) out of service, N2- | |||
SOP-08 directed that an orderly plant shutdown be commenced. Operators resumed | attempting to restore the 5C FWH to service, resultant system perturbations caused an | ||
power reduction until, at 50 percent power, the 6B FWH was successfully returned to | |||
service. The plant shutdown was terminated and power ascension commenced in | isolation of the 6C FWH. With two high pressure FWHs (6B and 6C) out of service, N2-SOP-08 directed that an orderly plant shutdown be commenced. Operators resumed | ||
coordination with restoration of the remaining affected systems. Power was restored to | |||
full RTP on July 15. The inspectors responded to the control room and observed operators' responses to the | power reduction until, at 50 percent power, the 6B FWH was successfully returned to | ||
service. The plant shutdown was terminated and power ascension commenced in | |||
coordination with restoration of the remaining affected systems. Power was restored to | |||
full RTP on July 15. | |||
The inspectors responded to the control room and observed operators' responses to the | |||
event, and reviewed the circumstances surrounding the event. | event, and reviewed the circumstances surrounding the event. | ||
b. Findings | |||
radioactive waste sump pump, caused an electrical transient that resulted in the loss of | ====b. Findings==== | ||
numerous plant components and required a power reduction. Description. In May of 2008, radioactive waste sump pump | |||
=====Introduction.===== | |||
WO required that a rotation check be performed after the | A self-revealing Green finding was identified on July 14, 2008, when inadequate maintenance practices, during replacement and troubleshooting of a Unit 2 | ||
electrical terminations had been completed. This, however, was not done because the | |||
radioactive waste sump pump, caused an electrical transient that resulted in the loss of | |||
numerous plant components and required a power reduction. | |||
=====Description.===== | |||
In May of 2008, radioactive waste sump pump 2DFW-P1A was replaced using a new model pump. The WO required that a rotation check be performed after the | |||
electrical terminations had been completed. This, however, was not done because the | |||
need for it was not recognized until after the pump had been installed in the sump. | need for it was not recognized until after the pump had been installed in the sump. | ||
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an | Although work was stopped to determine a course of action, the pump remained available | ||
for automatic operation as the backup sump pump. On July 8, 2008, it was recognized | |||
that the pump had run several times since the work had been stopped, as indicated by the | |||
pump run chart. This was incorrectly used to verify proper pump operation, and the | |||
rotation check and PMT steps in the WO were signed off as complete. | |||
On July 9, 2DFW-P1A was discovered to be running with no discharge pressure. In | |||
developing a troubleshooting plan, NMPNS initial actions were to reverse power leads to | |||
the pump. During testing the pump had no discharge pressure and, after two minutes, tripped on thermal overload. The leads were returned to the original configuration, and the pump was again energized by closing its circuit breaker on motor control center (MCC) | |||
2NHS-MCC016. Shortly after the breaker was shut, noise was heard and flame was | |||
observed coming from the breaker cubicle. | |||
The feeder breaker from power board 2NSH-US9 to 2NHS-MCC016 tripped; however, the undervoltage transient to 2NSH-US9, caused by this failure (a short), resulted in the equipment losses discussed above. | |||
In response to this event, the fire brigade responded to a fire alarm in the vicinity of 2NHS- | |||
MCC016. They found no fire and observ ed the damaged breaker for 2DFW-P1A. | |||
Operators responded to the partial loss of feedwater heating by reducing power to 73 | |||
percent. This issue was entered into the CAP as CR 2008-5745. | |||
The cause of the event was that the pump suction and discharge were plugged with debris | |||
from the sump, which resulted in high motor current due to the pump being in a bound 25 rotor condition. This, combined with a manufacturing defect associated with wiring | |||
insulation in the breaker, resulted in a phase-to-ground short between the breaker and the | |||
motor control center. | |||
The performance deficiency associated with this event was inadequate maintenance | |||
practices. Specifically: Following replacement in May, the pump was left in a condition | |||
such that it would operate automatically pr ior to the performance of PMT; and, the PMT | |||
was signed off based on pump run time rather than a verification of pump flow rate. | |||
NMPNS procedure GAP-SAT-02, "Pre/Post-Maintenance Test Requirements," Revision | |||
27, states that the PMT shall check components that were affected by the maintenance, verify that maintenance was properly performed, and verify that a new deficiency was not created. Had PMT been performed at the time of installation, low flow would likely have | |||
shown that the pump discharge piping was already plugged with sump debris. This would | |||
have prevented continued use of the pump and prevented subsequent troubleshooting | |||
from focusing on the direction of motor rotation. Additionally: The troubleshooting plan | |||
was inadequate in that, even if the pump had been rotating backwards, it would have | |||
developed some discharge pressure; and, after the phase reversal had produced no | |||
change in pump performance, the motor was restored to its original configuration and | |||
tested, rather than to have reevaluated the troubleshooting plan. Constellation procedure | |||
CNG-MN-1.01-1002, "Troubleshooting," Revision 0001, requires that troubleshooting shall | |||
be stopped in the event of an unexpected equipment response, and that the | |||
troubleshooting plan shall be reevaluated accordingly. | |||
=====Analysis.===== | |||
The finding was greater than minor because it was similar to IMC 0612, Appendix E, example 4.b, in that the inadequate maintenance resulted in a plant transient | |||
that affected multiple systems and components. The finding affected the human | |||
performance attribute of the Initiating Events cornerstone objective to limit the likelihood of | |||
those events that upset plant stability and challenge critical safety functions during | |||
shutdown as well as power operations. The finding was evaluated in accordance with IMC | |||
0609, Attachment 4, and determined to be of very low safety significance (Green) per the | |||
SDP Phase one determination because the finding did not contribute to both the likelihood | |||
of a rector trip and the likelihood that mitigation equipment or functions would not be | |||
available, and did not screen as potentially risk significant due to external events. | |||
The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appropriately plan the pump troubl eshooting activity by incorporating abort criteria (H.3.a per IMC 0305). | |||
=====Enforcement.===== | |||
No violation of regulatory requirements occurred. The inspectors determined that the finding did not represent a noncompliance issue because it occurred on non safety-class balance of plant equipment. (FIN 05000410/2008004-02, Inadequate Maintenance Practices Result in a Plant Transient)26 | |||
{{a|4OA5}} | |||
==4OA5 Other Activities== | |||
===.1 Quarterly Resident Inspector Observations of Security Personnel and Activities=== | |||
====a. Inspection Scope==== | |||
During the inspection period, the inspectors conducted observations of security force | |||
personnel and activities to ensure that the ac tivities were consistent with NMPNS's security procedures and regulatory requirements relating to nuclear plant security. These | |||
observations took place during both normal and off-normal plant working hours. | |||
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an | |||
integral part of the inspectors' normal plant status review and inspection activities. | integral part of the inspectors' normal plant status review and inspection activities. | ||
b. Findings | |||
====b. Findings==== | |||
No findings of significance were identified. | No findings of significance were identified. | ||
{{a|4OA6}} | |||
==4OA6 Meetings, including Exit== | |||
: | ===Exit Meeting Summary=== | ||
The inspectors presented the inspection results to Mr. Keith Polson and other members of | |||
NMPNS management on October 24, 2008. NM PNS acknowledged that no proprietary information was involved. | |||
ATTACHMENT: | |||
: [[ | |||
: | =SUPPLEMENTAL INFORMATION= | ||
: | |||
: [[ | ==KEY POINTS OF CONTACT== | ||
: | |||
: | ===Licensee Personnel=== | ||
: [[contact::S. Belcher]], Plant Manager | |||
: [[contact::W. Byrne]], Manager, Nuclear Security | |||
W. Byrne, Manager, Nuclear Security | : [[contact::R. Dean]], Director, Quality and Performance Assessment | ||
R. Dean, Director, Quality and Performance Assessment | : [[contact::T. Inc]], I&C Technician | ||
T. Inc, I&C Technician | : [[contact::J. Kaminski]], Manager, Emergency Preparedness | ||
J. Kaminski, Manager, Emergency Preparedness | : [[contact::J. Krakuszeski]], Manager, Operations | ||
J. Krakuszeski, Manager, Operations | : [[contact::J. Laughlin]], Manager, Engineering Services | ||
J. Laughlin, Manager, Engineering Services | : [[contact::K. Polson]], Vice President | ||
K. Polson, Vice President | : [[contact::J. Schultz]], Chemistry Supervisor, J.A. FitzPatrick Nuclear Power Plant | ||
J. Schultz, Chemistry Supervisor, J.A. FitzPatrick Nuclear Power Plant | : [[contact::T. Shortell]], Manager, Training | ||
T. Shortell, Manager, Training | : [[contact::S. Sova]], Manager, Radiation Protection | ||
S. Sova, Manager, Radiation Protection K. Stoffle, Environmental Support Supervisor J. Stone, Chemistry Technician | : [[contact::K. Stoffle]], Environmental Support Supervisor | ||
: [[T.]] | : [[contact::J. Stone]], Chemistry Technician | ||
: [[contact::T. Syrell]], Director, Licensing | |||
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED== | |||
===Opened and Closed=== | |||
: 05000410/2008004-01 NCV Incorrect Risk Assessment for RCIC Unavailability (Section 1R13) | |||
: 05000410/2008004-02 FIN Inadequate Maintenance Practices Result in | |||
a Plant Transient (Section 4OA3) | |||
RCIC Unavailability (Section 1R13) | ===Closed=== | ||
05000410/2008004-02 | : [[Closes LER::05000220/LER-2008-001]]-00 LER Loss of Offsite Power due to an Equipment | ||
: Malfunction (Section 4OA3) | |||
: [[Closes LER::05000410/LER-2008-001]]-00 LER Unqualified Relays Installed Since Original | |||
Closed | : Construction Result in an Unanalyzed | ||
05000220/2008-001-00 | : Condition (Section 4OA3) | ||
===Discussed=== | |||
05000410/2008-001-00 LER Unqualified Relays Installed Since Original Construction Result in an Unanalyzed | |||
Condition (Section 4OA3) | |||
Discussed | |||
None. | None. | ||
Attachment | |||
==LIST OF DOCUMENTS REVIEWED== | |||
==Section 1R01: Adverse Weather Protection== | |||
: | : S-ODP-OPS-0112, "Offsite Power Operations and Interface," Revision 12 | ||
: N1-SOP-33A.3, "Major 115 KV Grid Disturbances," Revision 01 | |||
: N2-SOP-70, "Major Grid Disturbances," Revision 01 | |||
: | : EPIP-EPP-26, "Natural Hazard Preparation and Recovery," Revision 01 | ||
: | : N1-OP-64, "Meteorological Monitoring," Revision 01 | ||
: | : N2-OP-102, "Meteorological Monitoring," Revision 04 | ||
Second Stage Cooling Pump and Fans," Revision 0000 | ==Section 1R04: Equipment Alignment== | ||
08-15377-00, "Implement Temp Mod to Provide to Cooling Bank Two from Transformer 1D" | : N2-ELU-01, "Walkdown Order Electrical Lineup and Breaker Operations," Revision 00 | ||
: | : N1-OP-18, "Service Water System," Revision 02 | ||
EC20080016-000 | : SDBD-502, "Service Water System Design Basis Document," Revision 07 | ||
Section 1R19: | : N1-ST-Q13, "Emergency Service Water Pump Operability Test," Revision 11 | ||
: | : N1-ST-V14, Service Water Check Valve And Emergency Service Water Pump and Check Valve Test," Revision 03 | ||
SAT-02, "Pre/Post Maintenance Test Requirements," Revision 26 | : N2-OP-33, "High Pressure Core Spray System," Revision 07 | ||
MDC-11, "Pump Curves and Acceptance Criteria," Revision 14 | : N2-VLU-01, "Walkdown Order Valve Lineup and Valv | ||
S15-72-F003, "IST Approved Pump Curves Emergency Diesel Generator Cooling Water," | e Operations," Attachment 33, "N2-OP-33 | ||
Revision 08 | : Walkdown Valve Lineup," Revision 00 | ||
N1-MMP-079-119, "Diesel Generator Cooling Water Pumps Maintenance," Revision 02 | : Piping and Instrumentation Diagram (P&ID)-33, "High Pressure Core Spray System" | ||
S-TTP-PUMP-@001, "Generic Pump Curve Validation Procedure," Revision 00 | |||
N2-OSP-SWP-@001, "Service Water Pump Curve Validation Test," Revision 04 | ==Section 1R05: Fire Protection== | ||
A10.1-N-341, "Revise | : NMPNS Unit 1 UFSAR, Appendix 10A, "Fire Hazards Analysis" | ||
: NMPNS Unit 2 UFSAR, Appendix 9A, "Degree of Compliance with Branch Technical Position | |||
IST Test Performance Flow Criteria From 9,000 to 10,000 | : CMEB 9.5-1" | ||
GPM," Revision 00, Disposition 00H | : NMPNS Unit 2 UFSAR, Appendix 9B, "Safe Shutdown Evaluation" | ||
N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability Test - Division I | : N2-FPI-PFP-0201, "Unit 2 Pre-Fire Plans," Revision 0 | ||
and | |||
==Section 1R06: Flood Protection Measures== | |||
: Internal Flooding Analysis Notebook, Nine Mile Point Unit 1, Revision 00 | |||
: Nine Mile Point Nuclear Station - Unit 1 Individual Plant Examination, July 1993 | |||
: N1-PM-V-29, "Reactor Building Sump Pump System Operability Test," Revision 00 | |||
: CR 2006-5956 | |||
: ACR 06-06589 | |||
==Section 1R07: Heat Sink Performance== | |||
: S15-79-HTX03, "Replacement Emergency Diesel Generator Raw Water Heat Exchanger Design," Revision 00 | |||
: S15-79-HTX-01, "Emergency Diesel Generator Cooling Water (EDGCW) Heat Exchanger Thermal Performance Evaluation," Revision 00, Disposition 00A | |||
: Attachment | |||
==Section 1R11: Licensed Operator Requalification Program== | |||
: N1-SOP-32, "Generator Auxiliaries Failures," Revision 02 | |||
: N1-SOP-33A.1, "Loss of 115 KV," Revision 01 | |||
: N1-SOP-33A.3, "Major 115 KV Grid Disturbances," Revision 01 | |||
: N1-EOP-2, "RPV Control," Revision 01400 | |||
: N1-EOP-4, "Primary Containment Control," Revision 01400 | |||
: N2-SOP-60, "Loss of Drywell Cooling," Revision 04 | |||
: N2-SOP-03, "Loss of AC Power," Revision 08 | |||
: N2-SOP-06, "Feed Water Failures," Revision 04 | |||
: N2-SOP-101D, "Rapid Power Reduction," Revision 05 | |||
: N2-SOP-29, "Sudden Reduction in Core Flow," Revision 07 | |||
: N2-SOP-101C, "Reactor Scram," Revision 03 | |||
: N2-EOP-RPV, "RPV Control," Revision 11 | |||
: N2-EOP-PC, "Primary Containment Control," Revision 12 | |||
: N2-EOP-C4, "RPV Flooding," Revision 12 | |||
==Section 1R12: Maintenance Effectiveness== | |||
: S-MRM-REL-0101, "Maintenance Rule," Revision 18 | |||
: S-MRM-REL-0104, "Maintenance Rule Scope," Revision 01 | |||
: S-MRM-REL-0105, "Maintenance Rule Performance Criteria," Revision 01 | |||
: Control Room HVAC System Health Reports, Q3-2006 through Q2-2008 | |||
: N2-TSP-HVC-R@001, "Testing and Analysis of Unit 2 Control Room Outdoor Air Special Filter Train System," Revision 01 | |||
: Reactor Recirculation System Health Reports, Q4-2007 through Q3-2008 | |||
: T-1792, "In-Place Testing of Nuclear Air Cleaning Systems for Nine Mile Point 2" Unit 2 Maintenance Rule Scoping Document | |||
: ASCR 08-04282 | |||
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control== | |||
: GAP-OPS-117, "Integrated Risk Management," Revision 14 | |||
: GAP-PSH-03, "Control of On-line Work Activities," Revision 15 | |||
: NAI-PSH-03, "On-line Work Management Process," Revision 11 | |||
==Section 1R15: Operability Evaluations== | |||
: CNG-OP-1.01-1002, "Conduct of Operability Determinations / Functionality Assessments," Revision 00 | |||
: A10.1-N-341, "Revise SWP Pump IST Test Performance Flow Criteria from 9000 GPM to | |||
: 10,000 GPM," Revision 00, Disposition 00H | |||
: N2-OSP-SWP-@001, "SW Pump Curve Validation Test," Revision 04 | |||
: Attachment Section R18: Plant Modifications | |||
: N1-MFT-105, "Replace CRD Timing Recorders," Revision 01 | |||
: C-22030-C, "Elementary Diagram Reactor Manual Control System," Sheet 1, Revision 33 | |||
: ESR 08-00812, "Raise 2SWP-TE-01 Setpoint to 150F for 2SWP*P1D" | |||
: CFR Part 50.59 Applicability Determination Form for | |||
: ESR 08-00812 | |||
: EC20080016-000, "Provide Alternate Power to the Main Step-Up Transformer 2MTX-XM1B | |||
: Second Stage Cooling Pump and Fans," Revision 0000 | |||
: 08-15377-00, "Implement Temp Mod to Provide to Cooling Bank Two from Transformer 1D" | |||
: CFR 50.59 Screening Form for EC20080016-000 | |||
==Section 1R19: Post Maintenance Testing== | |||
: GAP-SAT-02, "Pre/Post Maintenance Test Requirements," Revision 26 | |||
: MDC-11, "Pump Curves and Acceptance Criteria," Revision 14 | |||
: S15-72-F003, "IST Approved Pump Curves Emergency Diesel Generator Cooling Water," Revision 08 | |||
: N1-MMP-079-119, "Diesel Generator Cooling Water Pumps Maintenance," Revision 02 | |||
: S-TTP-PUMP-@001, "Generic Pump Curve Validation Procedure," Revision 00 | |||
: N2-OSP-SWP-@001, "Service Water Pump Curve Validation Test," Revision 04 | |||
: A10.1-N-341, "Revise SWP Pump IST Test Performance Flow Criteria From 9,000 to 10,000 | |||
: GPM," Revision 00, Disposition 00H | |||
: N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability Test - Division I | |||
and II," Revision 05 | |||
: N2-OP-100B, "HPCS Diesel Generator," Revision 08 | |||
==Section 1R22: Surveillance Testing== | |||
: CNG-HU-1.01, "Human Performance Program," Revision 01 | |||
: CNG-HU-1.01-1000, "Human Performance," Revision 02 | |||
: CNG-HU-1.01-1001, "Human Performance Tools and Verification Practices," Revision 02 | |||
: CNG-HU-1.01-1002, "Pre-Job Briefings and Post-Job Critiques," Revision 02 | |||
: GAP-SAT-01, "ST Program," Revision 16 | |||
: GAP-OPS-117, "Integrated Risk Management," Revision 14 | |||
: | |||
: | |||
: | |||
: | |||
: | |||
: | |||
==Section 1EP2: Alert and Notification System Evaluation== | |||
: Wyle Research Report | |||
: WR 82-26, "Qualification of the Oswego County Prompt Notification System for Nine Mile Point and James A. Fitzpatrick Nuclear Power Plants," | |||
: August 1982 | |||
: Wyle Research Report | |||
: WR 84-22, "Evaluation of the Oswego County Prompt Notification System," June 1984 | |||
: Public Notification System Service Manual, Federal Signal Corporation Engineered Systems | |||
: NMPNS | |||
: EPIP-EPP-30, "Prompt Notification System Problem Response," Revision 08 | |||
: NMPNS | |||
: EPMP-EPP-01, "Maintenance of Emergency Preparedness," Revision 24 | |||
: NMPNS | |||
: EPMP-EPP-08, "Maintenance, Testing and O | |||
peration of the Oswego County Prompt Notification System," Revision 14 | |||
: All siren and tone alert radio CRs dated between July 2006 and June 2008 | |||
: Attachment | |||
2006 | |||
2008 | |||
==Section 1EP3: Emergency Response Organization Staffing and Augmentation System== | |||
: [[ | : NMPNS Site Emergency Plan, Revision 54, Section 5, "Organization Control of Emergencies" | ||
: [[ | : NMPNS | ||
: [[ | : EPIP-EPP-13, "Emergency Response Facilities Activation and Operation," Revision 19 | ||
: [[ | : NMPNS | ||
: [[ | : EPMP-EPP-01, "Maintenance of Emergency Preparedness," Revision 24 | ||
: NMPNS | |||
: EPMP-EPP-06, "Emergency Response Organization Notification Maintenance and Surveillance," Revision 15 | |||
: NMPNS | |||
: GAP-OPS-01, "Administration of Operations," Revision 49 | |||
CFR | : Nine Mile Point Emergency Response Organization Duty Roster, Revision 2008-11 | ||
: NMPNS Training Server Emergency Preparedness Job Matrices | |||
CR | : Report, "Nine Mile Point Off-Hours Un-Announced All-Report Drill," October 12, 2007 | ||
CRD | : CR 2008-5135 | ||
DAC | |||
DBD | ==Section 1EP4: Emergency Action Level and Emergency Plan Changes== | ||
DC | : NMPNS Site Emergency Plan, Revision 54 | ||
DCP | : Licensing Document Change Request S-06-SEP-004 for Emergency Plan Revision 54 | ||
EAL | : NRC Safety Evaluation for NMPNS Site Emergency Plan Revision 54 | ||
EDG | : Change Packages for NMPNS Unit 1 EAL Revisions 16, 17, 18, and 19 | ||
: Change Package for NMPNS Unit 2 EAL Revision 15 | |||
: NMPNS | |||
: EPMP-EPP-01, "Maintenance of Emergency Preparedness," Revision 24, Attachment 3, "10CFR50.54(Q) Evaluation and Effectiveness Review" | |||
: CR 2007-7349 | |||
: 10CFR50.54(q) screenings and reviews, dated between August 2007 and June 2008 | |||
==Section 1EP5: Correction of Emergency Preparedness Weaknesses== | |||
: CNG-QL-101-1004, "Quality Audit Process," Revision 01 | |||
: October 2007 Report of Audit | |||
: EPP-07-01-N, Emergency Preparedness Program (10CFR50.54t Report) NMPNS Quality and Performance Assurance Assessment Reports: | |||
: 07-037, "ERO Staffing" | |||
: 07-054, "Observation of the June 7, 2007, EP Drill" | |||
: 07-068, "Observation of the NRC Graded EP Exercise and Follow-up Activities" | |||
: 08-005, "Use of Corrective Action Process in EP" | |||
: 08-006, "EAL Review" | |||
: 08-023, "Observation the of March 4, 2008, Drill" | |||
: 08-058, "Technical Support Center Focus Area Drills" | |||
: 08-064, "Observation of the June 26, 2008, Drill" | |||
: EP Oversight Board Minutes (various dates) | |||
: NMPNS Report for the September 19, 2007, Alert | |||
: NMPNS Report for the May 13, 2008, Unusual Event | |||
===Condition Report=== | |||
: Summary for all EP-related CRs dated between July 2007 and June 2008 | |||
==Section 1EP6: Drill Evaluation== | |||
: EPIP-EPP-01, "Classification of Emergency Conditions at Unit 1," Revision 17 | |||
: EPIP-EPP-20, "Emergency Notifications," Revision 18 | |||
==Section 2OS2: ALARA Planning and Controls== | |||
: NMP Unit 2 RFO11 Radiation Protection Post-Outage Report | |||
==Section 4OA1: Performance Indicator Verification== | |||
: NMPNS | |||
: EPMP-EPP-05, "Emergency Planning Program Self-Assessment," Revision 15 | |||
: Drill and Exercise Performance EP PI data, July 2007 - June 2008 | |||
: ERO Drill Participation PI data, July 2007 - June 2008 | |||
: Public Notification System PI data, July 2007 - June 2008 | |||
==Section 4OA2: Identification and Resolution of Problems== | |||
: CNG-CM-1.01-1003, "Design Engineering and Configuration Control", Revision 00001 | |||
: N2-ARP-1, Revision 00, Attachment 29 | |||
: CNG-MN-1.01-1006, "Oversight of Supplemental Personnel," Revision 00200 | |||
: CNG-CM-1.01-2003, "Acceptance of Vendor Engineering Products," Revision 0000 | |||
: NIP-CON-01, "Design and Configuration Control Process," Revision 23 | |||
: Safety Manual Chapter 20, Attachment | |||
: 4, "Electrical Safety Checklist" | |||
: WO 07-02412-18 | |||
===Condition Reports=== | |||
: 2008-5827 | |||
: 2008-5692 | |||
: 2008-5824 | |||
: 2008-5738 | |||
: 2008-6947 | |||
: 2008-7083 | |||
: 2008-7092 | |||
: 2008-7222 | |||
: 2008-7172 | |||
: 2008-5028 | |||
: 2008-6946 | |||
: 2008-6879 | |||
: 2008-6894 | |||
: 2008-6787 | |||
: 2008-6674 | |||
: 2008-6330 | |||
: 2008-4021 | |||
: 2008-6400 | |||
: 2008-6468 | |||
: 2008-6588 | |||
: 2008-6513 | |||
: 2008-6834 | |||
: 2008-7259 | |||
: 2004-3751 | |||
: 2006-1498 | |||
: 2006-4548 | |||
: 2006-4845 | |||
: 2006-5063 | |||
: 2006-5133 | |||
: 2006-5523 | |||
: 2006-5758 | |||
: 2007-0359 | |||
: 2007-0542 | |||
: 2007-0552 | |||
: 2007-1179 | |||
: 2007-1198 | |||
: 2007-5411 | |||
: 2007-6783 | |||
: 2007-7070 | |||
: 2008-0126 | |||
: 2008-0253 | |||
: 2008-1678 | |||
: 2008-1698 | |||
: 2008-2208 | |||
: 2008-3501 | |||
: 2008-4031 | |||
: 2008-4422 | |||
: 2008-4453 | |||
: 2008-5449 | |||
: 2008-6946 | |||
: 2008-7365 | |||
==LIST OF ACRONYMS== | |||
: [[AC]] [[alternating current]] | |||
ADAMS Agency Documents | |||
Access Management System | |||
: [[ALARA]] [[as low as reasonably achievable]] | |||
: [[ANS]] [[alert and notification system]] | |||
: [[CAP]] [[corrective action program]] | |||
: [[CDF]] [[core damage frequency]] | |||
: [[CFR]] [[Code of Federal Regulations]] | |||
: [[CO]] [[2 carbon dioxide]] | |||
: [[CR]] [[condition report]] | |||
: [[CRD]] [[control rod drive]] | |||
: [[DAC]] [[derived air concentration]] | |||
: [[DBD]] [[design basis document]] | |||
: [[DC]] [[direct current]] | |||
: [[DCP]] [[design change package]] | |||
: [[EAL]] [[emergency action level]] | |||
: [[EDG]] [[emergency diesel generator]] | |||
: [[EOP]] [[emergency operating procedure]] | : [[EOP]] [[emergency operating procedure]] | ||
: [[EP]] [[emergency preparedness]] | : [[EP]] [[emergency preparedness]] | ||
ERO | : [[ERO]] [[emergency response organization]] | ||
ESW emergency service water | |||
F Fahrenheit | F Fahrenheit | ||
: [[FWH]] [[feedwater heater]] | : [[FWH]] [[feedwater heater]] | ||
HPCS high pressure core spray | |||
hr hour | hr hour | ||
: [[ | : [[HVAC]] [[heating, ventilation, and air conditioning]] | ||
: [[IA]] [[instrument air]] | : [[IA]] [[instrument air]] | ||
: [[ | : [[ICDP]] [[incremental core damage probability]] | ||
IMC inspection manual chapter | IMC inspection manual chapter | ||
kV kilovolt | kV kilovolt | ||
LCV | : [[LCV]] [[level control valve]] | ||
: [[LER]] [[licensee event report]] | : [[LER]] [[licensee event report]] | ||
: [[ | : [[LORT]] [[licensed operator requalification training]] | ||
MCC motor control center | MCC motor control center | ||
mrem millirem | mrem millirem | ||
NCV | : [[NCV]] [[non-cited violation]] | ||
: [[NEI]] [[Nuclear Energy Institute]] | : [[NEI]] [[Nuclear Energy Institute]] | ||
: [[NMPNS]] [[Nine Mile Point Nuclear Station,]] | : [[NMPNS]] [[Nine Mile Point Nuclear Station,]] | ||
| Line 1,313: | Line 1,620: | ||
: [[NRC]] [[Nuclear Regulatory Commission]] | : [[NRC]] [[Nuclear Regulatory Commission]] | ||
: [[OE]] [[operating experience]] | : [[OE]] [[operating experience]] | ||
: [[ | : [[PARS]] [[Publicly Available Records]] | ||
: [[PI]] [[performance indicator]] | |||
PI | : [[PMT]] [[post maintenance test]] | ||
PMT | |||
: [[RB]] [[reactor building]] | : [[RB]] [[reactor building]] | ||
: [[ | : [[RCIC]] [[reactor core isolation cooling]] | ||
RHR residual heat removal | |||
RHR residual heat removal | |||
A-8RPV reactor pressure vessel RRP | A-8RPV reactor pressure vessel | ||
RTP | : [[RRP]] [[reactor recirculation pump]] | ||
SDP | : [[RTP]] [[rated thermal power]] | ||
SOP | : [[SDP]] [[significance determination process]] | ||
SW | : [[SOP]] [[special operating procedure]] | ||
TI | : [[SW]] [[service water]] | ||
: [[TI]] [[temporary instruction]] | |||
: [[TS]] [[technical specification]] | : [[TS]] [[technical specification]] | ||
: [[ | : [[UFSAR]] [[updated final safety analysis report]] | ||
: [[UPS]] [[uninterruptible power supply]] | |||
UPS | |||
WO work order | WO work order | ||
yr year | yr year | ||
}} | }} | ||
Revision as of 07:04, 28 August 2018
| ML083101203 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 11/05/2008 |
| From: | Dentel G T Reactor Projects Branch 1 |
| To: | Polson K J Nine Mile Point |
| Dentel, G RGN-I/DRP/BR1/610-337-5233 | |
| References | |
| IR-08-004 | |
| Download: ML083101203 (38) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406-1415 November 5, 2008
Mr. Keith Vice President Nine Mile Point
Nine Mile Point Nuclear Station, LLC
P.O. Box 63
Lycoming, NY 13093
SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000220/2008004 and 05000410/2008004
Dear Mr. Polson:
On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an
inspection at your Nine Mile Point Nuclear Station, Units 1 and 2. The enclosed integrated
inspection report documents the inspection results discussed on October 24, 2008, with you and
members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents one self-revealing finding and one NRC-identified finding of very low
safety significance (Green). One of the findings was determined to involve a violation of NRC
requirements. However, because of its very low safety significance and because it was entered
into your corrective action program (CAP), the NRC is treating this violation as a non-cited
violation in accordance with Section VI.A.1 of the NRC's Enforcement Policy. If you contest the
non-cited violation noted in this report, you should provide a response with the basis for your
denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory
Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to the
Regional Administrator, Region I; the Director, Office of Enforcement; U.S. Nuclear Regulatory
Commission, Washington, D.C. 20555-001; and the NRC Senior Resident Inspector at Nine Mile Point Nuclear Station.
In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Public ly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/ Glenn T. Dentel, Chief Projects Branch 1
Division of Reactor Projects Docket No.: 50-220, 50-410 License No.: DPR-63, NPF-69
Enclosure:
Inspection Report 05000220/2008004 and 05000410/2008004
w/Attachment:
Supplemental Information
cc w/encl:
M. Wallace, Vice - Chairman, Constellation Energy
H. Barron, President, CEO & Chief Nuclear Officer, Constellation Energy Nuclear Group
C. Fleming, Esquire, Senior Counsel, Nuclear Generation, Constellation Energy Group, LLC M. Wetterhahn, Esquire, Winston & Strawn
T. Syrell, Director, Licensing, Nine Mile Point Nuclear Station
P. Tonko, President and CEO, New York State Energy Research and Development Authority
J. Spath, Program Director, New York State Energy Research and Development Authority
P. Eddy, New York State Department of Public Service
C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law
Supervisor, Town of Scriba
P. Church, Oswego County Administator
T. Judson, Central NY Citizens Awareness Network
D. Katz, Citizens Awareness Network
G. Detter, Manager, Nuclear Safety and Security, Constellation Energy
SUMMARY OF FINDINGS
IR 05000220/2008004, 05000410/2008004; 07/01/08 - 09/30/08; Nine Mile Point Nuclear Station,
Units 1 and 2; Maintenance Risk Assessment and Event Followup.
The report covered a three-month period of inspection by resident inspectors and regional specialist inspectors. One Green non-cited violation (NCV), and one Green finding, were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process (SDP)."
Findings for which the SDP does not apply may be Green or be assigned a severity level after
NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Initiating Events
- Green.
A self-revealing finding was identified on July 14, 2008, when inadequate maintenance practices, during replacement and troubleshooting of a Unit 2 radioactive waste sump pump, caused an electrical transient that resulted in the loss of numerous plant components and required a power reduction. The inadequate maintenance practices included failure to perform post-maintenance testing and continuation of troubleshooting despite having obtained results that were not consistent with the troubleshooting plan. This issue was entered into NMPNS's corrective action program for evaluation.
The finding was greater than minor because it affected the human performance attribute of the Initiating Events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The finding was evaluated in accordance with IMC 0609 and determined to be of very low safety significance because the finding did not contribute to both the likelihood of a rector trip and the likelihood that mitigation equipment or functions would not be available, and did not screen as potentially risk significant due to external events. The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appropriately plan the pump troubleshooting activity by incorporating abort criteria (H.3.a per IMC 0305). (Section 4OA3)
Cornerstone: Mitigating Systems
- Green.
An NRC-identified non-cited violation (NCV) of 10 CFR 50.65(a)(4) was identified for inaccurate risk assessments completed for August 5 and 6, 2008.
Specifically, the unavailable reactor core isolation cooling (RCIC) system was not properly incorporated into the risk assessment. The cause was determined to be that an error had been made while entering a change to the risk monitor computer software, which resulted in RCIC incorrectly being assigned a zero risk importance.
As corrective actions, the modeling of RCIC was corrected and a verification of all mapping codes used in the risk monitor was performed.
The finding was greater than minor because the risk assessment for RCIC system maintenance was inadequate due to inaccurate information that was provided to the risk assessment tool. As a result, the ov erall elevated plant risk, when correctly assessed, put the plant into a higher licensee-established risk category. The finding was evaluated in accordance with IMC 0609, Appendix K, and determined to be of very low safety significance because the incremental core damage probability deficit (ICDPD) was less than 1E-6. The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appr opriately plan work activities by incorporating valid risk insights (H.3.a per IMC 0305). (Section 1R13)
B. Licensee-Identified Violations
None.
5
REPORT DETAILS
Summary of Plant Status
Nine Mile Point Unit 1 began the inspection period at full rated thermal power (RTP). Several
short duration power reductions were performed for maintenance on reactor recirculation pump (RRP) motor-generators, and on September 27, power was reduced to 68 percent for a control
rod sequence exchange, single rod scram time testing, and turbine valve testing. Power was
restored to 100 percent the following day, and remained there for the rest of the inspection period.
Nine Mile Point Unit 2 began the inspection period at full RTP. On July 14, power was reduced to
50 percent due to loss of two high pressure feedwater heaters (FWHs), which resulted from an
electrical transient due to an equipment failure. The FWHs were subsequently returned to
service, and power was restored to 100 percent t he next day. On September 4, an increase in drywell airborne radioactive particulate activity, along with indication of a slowly degrading pump seal for the 'B' RRP and an apparent rapid increase in drywell unidentified leakage, prompted operators to perform a rapid power reduction to 93 percent. It was later determined that drywell
leakage was actually unchanged and stable, as were 'B' RRP seal parameters. Power was
restored to full RTP later that day. On September 18, power was reduced to 86 percent due to a problem with the main transformer cooling system. The problem was resolved and power was
restored to full RTP later that day. Unit 2 continued to operate at full RTP for the remainder of the
inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01 - One sample)
a. Inspection Scope
On July 24, 2008, the inspectors reviewed NMPNS's actions in response to a severe
electrical storm in the vicinity of the station. During this storm, Unit 1 experienced a
momentary loss of one of the two 115 kilovolt (kV) offsite power lines (line 1) due to a
lightning strike. Offsite power continued to be supplied to both vital switchboards from
offsite line 4, so this event did not result in an automatic start of the associated emergency
diesel generator (EDG). The affected breaker, onsite supply breaker R-10, automatically
reclosed as designed after approximately 5 seconds. The event did not have any
significant effect on plant operations. The inspectors verified that operators implemented
actions specified in the associated procedure to reduce the impact that the adverse
weather had on the site. The inspectors also verified that the NMPNS procedures addressed measures to monitor and maintain availability and reliability of the other offsite alternating current (AC) power system and t he onsite alternate AC power system during adverse weather conditions.
b. Findings
6 No findings of significance were identified.
1R04 Equipment Alignment
.1 Partial System Walkdown (71111.04 - Four samples)
a. Inspection Scope
The inspectors performed partial system walkdowns to verify risk-significant systems were
properly aligned for operation. The inspectors verified the operability and alignment of
these risk-significant systems while their r edundant trains or systems were inoperable or
out of service for maintenance. The inspec tors compared system lineups to system operating procedures, system drawings, and the applicable chapters in the updated final
safety analysis report (UFSAR). The inspectors verified the operability of critical system
components by observing component material condition during the system walkdown.
The inspectors performed partial walkdowns of the following systems:
- Unit 1 core spray system 111 while core spray system 112 was inoperable for in-service testing;
- Unit 1 core spray system 12 while the 112 core spray topping pump was inoperable and unavailable for maintenance;
- Unit 2 125 volt direct current (DC) electrical system, Divisions 1 and 2, due to high safety significance; and
- Unit 2 high pressure core spray (HPCS) system while the reactor core isolation cooling (RCIC) system was inoperable for maintenance.
b. Findings
No findings of significance were identified.
.2 Complete System Walkdown (71111.04S - One sample)
a. Inspection Scope
The inspectors performed a complete walkdown of the Unit 1 emergency service water (ESW) system to identify discrepancies between the existing equipment configuration and
that specified in the design documents. During the walkdown, system drawings and
operating procedures were used to determine the proper equipment alignment and
operational status. The inspectors reviewed the open maintenance work orders (WOs)
that could affect the ability of the system to perform its functions. Documentation
associated with temporary modifications, operator workarounds, and items tracked by
plant engineering were also reviewed to assess their collective impact on system
operation. In addition, the inspectors reviewed the condition report (CR) database to
verify that equipment alignment problems were being identified and appropriately
resolved.
b. Findings
7 No findings of significance were identified.
1R05 Fire Protection
.1 Quarterly Inspection (71111.05Q - Six samples)
a. Inspection Scope
The inspectors toured areas important to reactor safety at NMPNS to evaluate the
station's control of transient combustibles and ignition sources, and to examine the
material condition, operational status, and operational lineup of fire protection systems
including detection, suppression, and fire barriers. The areas inspected included:
- Unit 1 reactor building (RB) 261 foot elevation;
- Unit 1 RB 281 foot elevation;
- Unit 1 emergency cooling system steam isol ation valve room, RB 298 foot elevation;
- Unit 2 RB 261 foot elevation;
- Unit 2 RB 289 foot elevation; and
- Unit 2 RB 353 foot elevation.
b. Findings
No findings of significance were identified.
.2 Annual Inspection (71111.05A - One sample)
a. Inspection Scope
The inspectors completed one annual fire drill observation inspection sample. The
inspectors observed a fire brigade drill on September 17, 2008, in the Unit 1 turbine
building. The inspectors observed brigade performance during the drill to evaluate
donning and use of protective equipment and self-contained breathing apparatus, fire
brigade leader command and control, fire brigade response time, communications, and
the use of pre-fire plans. The inspectors attended the post-drill critique and reviewed the
disposition of issues and deficiencies identified during the drill.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures (71111.06 - One sample)
a. Inspection Scope
The inspectors completed one internal flooding sample. The inspectors reviewed the
individual plant examination and UFSAR for Unit 1 concerning internal flooding events and
completed walkdowns of one area in which flooding could have a significant impact on
risk. The RB torus room and the RB northwest corner room were reviewed.
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance (71111.07A - One sample)
a. Inspection Scope
The inspectors reviewed maintenance records for Unit 1 102 EDG cooling water heat
exchangers 79-03 and 79-04, performed in acco rdance with N1-MPM-079-412, "Diesel Generator Cooling Water Heat Exchanger and Temperature Control Valve Maintenance."
The inspectors reviewed EDG performance data to verify that heat exchanger operation
was consistent with the design basis. The inspectors interviewed the system engineer to
verify overall condition of the heat exchangers.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification Program (71111.11Q - Two samples)
a. Inspection Scope
The inspectors evaluated two simulator scenarios in the licensed operator requalification
training (LORT) program. The inspectors assessed the clarity and effectiveness of
communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operation, and the oversight and direction provided by
the shift manager. During the scenario, the inspectors also compared simulator
performance with actual plant performance in the control room. The following scenarios
were observed:
- On August 26, 2008, the inspectors observed Unit 1 LORT to assess operator and instructor performance during a scenario involving a main generator hydrogen seal oil pump failure, a grid transient that resulted in a loss of offsite 115 kV power with failure
of the 103 EDG to start, a loss of coolant accident, and failure of the reactor vessel
fuel zone water level indicator. The inspectors evaluated the performance of risk
significant operator actions including the use of special operating procedures (SOPs)
and emergency operating procedures (EOPs).
9
- On 5 September, 2008, the inspectors observed Unit 2 LORT to assess operator and instructor performance during a scenario involving a loss of drywell cooling, a loss of normal power to the Division 1 and 3 electrical busses, high motor temperature on one
of the operating reactor feedwater pumps that led to loss of the pump, and a loss of
coolant accident in the drywell along with failure of all reactor pressure vessel (RPV)
level indication, requiring RPV flooding. The inspectors evaluated the performance of
risk significant operator actions including the use of SOPs and EOPs.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12Q - Three samples)
a. Inspection Scope
The inspectors reviewed performance-based problems and the performance and condition
history of selected systems to assess the effectiveness of the maintenance program. The
inspectors reviewed the systems to ensure that the station's review focused on proper
maintenance rule scoping in accordance with 10 CFR Part 50.65, characterization of
reliability issues, tracking system and component unavailability, and 10 CFR Part 50.65 (a)(1) and (a)(2) classification. In addition, the inspectors reviewed the site's ability to
identify and address common cause failures and to trend key parameters. The following
four maintenance rule inspection samples were reviewed:
- Unit 2 control building heating, ventilation, and air conditioning (HVAC) system based on equipment problems that developed following implementation of a modification; and
- Unit 2 reactor recirculation system based on recirculation pump seal leakage issues.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - Six samples)
a. Inspection Scope
The inspectors evaluated the effectiveness of the maintenance risk assessments required
by 10 CFR Part 50.65 (a)(4). The inspectors reviewed equipment logs, work schedules, and performed plant tours to verify that actual plant configuration matched the assessed
configuration. Additionally, the inspectors verified that risk management actions for both
planned and emergent work were consistent with those described in station procedures.
The inspectors reviewed risk assessments for the activities listed below.
Unit 1 10
- Week of July 14, 2008, that included a rebuild of 112 core spray topping pump, 13 turbine building closed loop cooling system heat exchanger cleaning, and emergent
maintenance to troubleshoot a trip of the 13 instrument air (IA) compressor, combined
within a scheduled maintenance period.
- Week of July 21, 2008, that included 112 containment spray raw water system maintenance and quarterly surveillance, 102 EDG monthly surveillance, and emergent issues with reactor protection system UPS 162B that resulted in a half scram signal, and loss of flow monitoring capability for the electromatic relief valves and safety
valves due to a failed power supply.
- Week of August 18, 2008, that included maintenance on the 13 RRP motor-generator, a power reduction to 85 percent for recovery of 13 RRP, and emergent maintenance to
replace the 103 EDG raw water pump due to low discharge pressure.
Unit 2
- Week of July 14, 2008, that included Division 1 EDG monthly surveillance, residual heat removal (RHR) 'A' quarterly surveillance, replacement of unannealed red brass
piping in the IA system, and emergent maintenance to troubleshoot a level control
problem with the 2B low pressure FWH, and troubleshooting activities associated with
a radioactive waste sump pump that resulted in multiple plant equipment issues and
required a power reduction to 50 percent.
- Week of July 21, 2008, that included HPCS system maintenance and quarterly surveillance, a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run of the Division 3 EDG for a two year surveillance, and
emergent maintenance to troubleshoot Division 3 EDG voltage oscillations, a level control problem with the 2B low pressure FWH, and a leak from the low pressure core spray pressure maintenance (keepfill) pump mechanical seal water supply.
- Week of August 4, 2008, that included inspection of the 'B' IA dryer, maintenance on the 'C' IA compressor, weld repair of the 'C' IA receiver, a three day maintenance
period on the RCIC system, and RCIC quarterly surveillance.
b. Findings
Introduction.
An NRC-identified Green NCV of 10 CFR 50.65(a)(4) was identified for inaccurate risk assessments completed for August 5 and 6, 2008. Specifically, the
unavailable reactor core isolation cooling (RCIC) system was not properly incorporated into the risk assessment.
Description.
During the week of August 4, 2008, the RCIC system was made inoperable and unavailable on several occasions for planned maintenance activities. When the
inspectors reviewed NMPNS's daily risk assessment on August 6, they noted that RCIC
would be inoperable and unavailable and that the value for daily CDF risk was indicated to
be "Low." The inspectors questioned this, based on previous experience when RCIC
having been unavailable had caused the daily CDF risk to be "Medium." On August 8, 11 NMPNS determined that the daily CDF risk should have been "Medium" while RCIC was
inoperable and unavailable. Prior to this determination, RCIC had been inoperable and
unavailable on two occasions during the week, with a total unavailability time of
approximately 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> (hrs).
The cause of the incorrect risk assessment was determined to be that a typographical
error had been made on June 30, 2008, while entering a change to the risk monitor
computer software. This resulted in an error in the coding used to map RCIC
unavailability to risk importance in the Unit 2 PRA model, incorrectly giving it a zero risk
importance. As corrective actions, the modeling of RCIC was corrected and a verification of all mapping codes used in the risk monitor was performed. This issue was entered into the corrective action program (CAP) as CR 2008-6363.
The performance deficiency associated with this event was that inaccurate information
was entered in the risk monitor software resulting in an inadequate risk assessment being
used while the RCIC system was inoperable and unavailable during the August 4, 2008
work week.
Analysis.
The finding was greater than minor because it was similar to IMC 0612, Appendix E, example 7.e, in that the risk assessment for RCIC system maintenance was
inadequate (i.e., it underestimated the risk because of personnel error) because relevant
information provided to the risk assessment tool was inaccurate. As a result, the overall
elevated plant risk, when correctly assessed, put the plant into a higher licensee-
established risk category. Per IMC 0609, Attachment 4, Phase 1, "Initial Screening and
Characterization of Findings," the finding was evaluated in accordance with IMC 0609, Appendix K, "Maintenance Risk Assessment and Risk Management Significance
Determination Process." The baseline (zero-maintenance) core damage frequency was
1.35E-5/year (yr) and the actual core damage frequency (with RCIC unavailable) was
5.10E-5/yr. Therefore, the actual incremental core damage frequency was (5.10 - 1.35)E-
5/yr = 3.75E-5/yr, and the actual incremental core damage probability (ICDP actual) was (3.75E-5/yr x 30 hrs) / 8760 hrs/yr = 1.28E-7. Although a risk assessment had been
performed, the value was essentially the zero-maintenance core damage frequency; that
is, it was evaluated the same as if a risk assessment had not been performed. Therefore, the incremental core damage probability deficit (ICDPD) was equal to ICDP actual. Since ICDPD was less than 1E-6, the finding was determined to be of very low safety
significance (Green).
The finding had a cross-cutting aspect in the area of human performance because
NMPNS did not appropriately plan work activities by incorporating valid risk insights (H.3.a
per IMC 0305).
Enforcement.
10 CFR 50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear power plants," subsection (a)(4) states, in part, "Before performing
maintenance activities . . . the licensee shall assess and manage the increase in risk that
may result from the proposed maintenance activities. The scope of the
assessment may be limited to structures, sy stems, and components that a risk-informed evaluation process has shown to be significant to public health and safety." The NMPNS 12 Maintenance Rule Manual classifies the Unit 2 RCIC system as a high safety significant system. Contrary to the above, on August 8, 2008, it was identified that NMPNS had not correctly
assessed the risk associated with maintenance activities on August 5 and August 6 that
had made the Unit 2 RCIC system inoperable and unavailable, in that the daily CDF risk
had been determined to be "Low" when the actual value was "Medium." Because this
violation is of very low safety significance and was entered into the CAP as CR 2008-
6363, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000410/2008004-01, Incorrect Risk Assessment for RCIC Unavailability)
1R15 Operability Evaluations (71111.15 - Seven samples)
a. Inspection Scope
The inspectors evaluated the acceptability of operability evaluations, the use and control
of compensatory measures, and compliance with technical specifications (TSs.) The
evaluations were reviewed using criteria specified in NRC Regulatory Issue Summary
2005-20, "Revision to Guidance Formerly Contained in NRC Generic Letter 91-18,
'Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution
of Degraded and Nonconforming Conditions and on Operability'," and Inspection Manual
Part 9900, "Operability Determinations and Functionality Assessments for Resolution of
Degraded or Nonconforming Conditions Adverse to Quality or Safety." The inspectors'
review included verification that the operability determinations were made as specified by
Procedure CNG-OP-1.01-1002, "Conduct of Operability Determinations / Functionality
Assessments." The technical adequacy of the determinations was reviewed and compared to the TSs, UFSAR, and associated design basis documents (DBDs).
The following evaluations were reviewed:
- CR 2008-5852 concerning the operability of the Unit 1 drywell equipment drain tank input to the drywell leak detection system, in light of anomalous tank level and leak rate indications;
- CR 2008-6536 concerning degraded flow from the Unit 1 EDG 103 raw water pump, identified during its quarterly surveillance;
- CR 2008-6643 concerning water and sediment in Unit 1 EDG fuel oil storage tank bottom samples;
- CR 2008-5841 concerning degraded performance of one of the Unit 2 'A' RHR pump room unit coolers;
- CR 2008-5439 concerning operability of the Unit 2 Division 2 EDG in the emergency mode with a failed overspeed butterfly valve limit switch that had caused the EDG to shut down while operating in the test mode;
- CR 2008-5885 concerning the effect of increased Unit 2 suppression pool leakage on emergency core cooling system pump operability; and
- CR 2008-6647 concerning low peak firing pressure on one cylinder for the Unit 2 Division 3 EDG.
b. Findings
No findings of significance were identified.
1R18 Plant Modifications (71111.18 - Four samples)
.1 Temporary Modifications
a. Inspection Scope
The inspectors reviewed a Unit 2 temporary modification to raise the 'D' service water
pump outboard bearing temperature setpoint from 130 degrees Fahrenheit (F) to 150 F.
The setpoint was raised to allow for new packing run-in on the pump. The inspectors
reviewed the 10 CFR Part 50.59 screening against the system design bases
documentation to verify that the modification did not affect system operability. The
inspectors reviewed the vendor manual to verify that increased temperature would not
affect the pump's reliability.
The inspectors reviewed a Unit 2 temporary modification that installed temporary power to
the B-phase main transformer cooling pumps and fans from the installed spare 'D' main
transformer. The inspectors reviewed the at-risk activity work package, interviewed the system engineer, and reviewed the 10 CFR Part 50.59 screening against the system design bases documentation to verify that the modification did not affect system
operability. The inspectors also reviewed the WO that installed and removed the
temporary power and walked down the equipment after work completion to verify that the
equipment had been returned to its original configuration.
b. Findings
No findings of significance were identified.
.2 Permanent Modifications
a. Inspection Scope
The inspectors reviewed Unit 2 design change package (DCP) N2-99-032, "Gaseous
Effluent Monitoring System Replacement."
The purpose of this modification was to replace an aging system for which system reliability had been degrading. The inspectors
assessed the adequacy of the modification package and procedural changes, verified that
applicable design and licensing basis requirements were met, and verified that design
margins were not degraded by the modification.
The inspectors reviewed Unit 1 DCP N1-08-013, "Replace Control Rod Drive (CRD)
Timing Recorders at NMP1." The purpose of this modification was to improve the process
by which data is acquired and analyzed for all control rod movement. The inspectors
assessed the adequacy of the modification package and 10 CFR Part 50.59 screening, verified that applicable design and licensing basis requirements were met, and verified that design margins were not degraded by the modification. The inspectors interviewed
engineers involved with the project, walked down the system, and reviewed the post-14 maintenance test (PMT) results to verify proper installation and the test acceptance criteria
had been met. The inspectors also reviewed the affected procedures and drawings to
verify that affected documents were being updated.
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing (71111.19 - Seven samples)
a. Inspection Scope
The inspectors reviewed the PMTs listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test
procedure to verify that the procedure adequately tested the safety functions that may
have been affected by the maintenance activity, that the acceptance criteria in the
procedure were consistent with information in the applicable licensing basis and/or DBDs, and that the procedure had been properly reviewed and approved. The inspectors also
witnessed the test or reviewed test data, to verify that the test results adequately
demonstrated restoration of the affected safety functions.
.
- Unit 1, WO 08-11429-00 that replaced capacitors in uninterruptable power supply UPS-162A. The PMT was performed in accordance with N1-EPM-UPS-003, "UPS 10
Year Maintenance," and a 24-hour confidence run.
- Unit 1, WO 08-13901-00 that replaced the EDG 103 raw water pump. The PMT was performed in accordance with N1-ST-Q25, "EDG Cooling Water Quarterly Test," and N1-PM-V2, "Pump Curve Validation Test."
- Unit 1, WO 08-09002-00 that rebuilt the 112 core spray topping pump. The PMT was performed in accordance with N1-ST-Q1C, "Core Spray 112 Pump and Valve
Operability Test," and N1-PM-V2, "Pump Curve Validation Test."
- Unit 1, WO 06-20738-00 that performed preventive maintenance on stack off-gas radiation monitor, RAM-112-08A. The PMT was performed in accordance with N1-
ISP-112-001, "Stack Gas Monitor Calibration."
- Unit 2, ACR 08-04217 that performed troubleshooting of the Division 2 EDG overspeed butterfly valve limit switch fa ilure. The PMT was performed in accordance with N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability
Test - Division I and II."
- Unit 2, ACR 08-04603 that performed troubleshooting of the Division 3 EDG voltage regulator motor operated potentiometer. The PMT was performed in accordance with N2-OP-100B, "HPCS Diesel Generator."
- Unit 2, WO 06-13888-00 that rebuilt service water pump 2SWP*P1D. The PMT was 15 performed in accordance with N2-OSP-SWP-@001, "Service Water Pump Curve
Validation Test."
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing (71111.22 - Eight samples)
a. Inspection Scope
The inspectors witnessed performance of and/or reviewed test data for risk-significant
surveillance tests to assess whether the components and systems tested satisfied design and licensing basis requirements. The inspectors verified that test acceptance criteria
were clear, demonstrated operational readiness and were consistent with the DBDs; that
test instrumentation had current calibrations and the range and accuracy for the
application; and that tests were performed, as written, with applicable prerequisites
satisfied. Upon test completion, the inspectors verified that equipment was returned to the
status specified to perform its safety function.
The following surveillance tests were reviewed:
- N1-ST-Q2, "Control Rod Drive Pumps Flow Rate Test;"
- N1-ST-Q13, "Emergency Service Water Pump Operability Test;"
- N1-ST-M4A, "EDG 102 and PB 102 Operability Test;"
- N1-ST-Q6A, "Containment Spray System Loop 111 Quarterly Operability Test;"
- N2-PM-A006, "B.5.b Pump Annual Flow Rate Test;"
- N2-OSP-ICS-Q@002, "RCIC Pump and Valve Operability Test and System Integrity Test and ASME XI Functional Test;"
- N2-OSP-SWP-Q@001, "Division 1 SW Operability Test;" and
- N2-TSP-HVC-R@001, "Testing and Analysis of Unit 2 Control Room Outdoor Air Special Filter Train System."
b. Findings
No findings of significance were identified.
16 Cornerstone: Emergency Preparedness 1EP2 Alert and Notification System Evaluation (71114.02 - One sample)
a. Inspection Scope
An onsite review was conducted to assess the maintenance and testing of the NMPNS
alert and notification system (ANS), including both the system sirens and tone alert radios.
During this inspection, the inspectors interviewed emergency preparedness (EP) staff
responsible for implementation of the ANS testing and maintenance. The inspectors
reviewed CRs pertaining to the ANS for causes, trends, and NMPNS's corrective actions.
The inspectors further discussed the ANS with the assigned technical specialist, reviewing
system performance from June 2006 through June 2008. The inspectors reviewed the
ANS procedures and the ANS design report to ensure NMPNS's compliance with those
commitments for system maintenance and testing. Additionally, the inspectors reviewed
changes to the design report and how these changes were captured. The Planning
Standard, 10 CFR Part 50.47(b)(5), and the related requirements of 10 CFR Part 50, Appendix E, were used as reference criteria.
b. Findings
No findings of significance were identified.
1EP3 Emergency Response Organization Staffing and Augmentation System (71114.03 - One sample)
a. Inspection Scope
The inspectors conducted a review of the NMPNS emergency response organization (ERO) augmentation staffing requirements and the process for notifying and augmenting
the ERO. This was performed to ensure the readiness of key staff for responding to an
event and to ensure timely facility activation. The inspectors reviewed procedures and
CRs associated with the ERO notification system and drills, and reviewed records from
call-in drills. The inspectors interviewed personnel responsible for testing the ERO
augmentation process, and reviewed the training records for a sampling of ERO to ensure
training and qualifications were up to date. The inspectors reviewed procedures for ERO
administration and training, and verified a sampling of ERO participation in exercises and
drills in 2007 and 2008. The Planning Standard, 10 CFR Part 50.47(b)(2) and related requirements of 10 CFR Part 50, Appendix E, were used as reference criteria.
b. Findings
No findings of significance were identified.
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - One sample)
a. Inspection Scope
Prior to this inspection, the NRC had received and acknowledged changes made to the
NMPNS emergency plan and its implementi ng procedures. NMPNS developed these changes in accordance with 10 CFR Part 50.54(q), and determined that the changes did
not result in a decrease in effectiveness of the NMPNS Site Emergency Plan (the Plan).
NMPNS also determined that the Plan continued to meet the requirements of 10 CFR Part
50.47(b) and Appendix E to 10 CFR Part 50. During this inspection, the inspectors
conducted a review of NMPNS
=s 10 CFR Part 50.54(q) screenings for all the changes made to the emergency action levels (EALs) and all of the changes made to the Plan from
August 2007 through June 2008 that could have potentially resulted in a decrease in effectiveness of the Plan. This review of the EALs and Plan changes did not constitute NRC approval of the changes and, as such, the changes remain subject to future NRC
inspection. The requirements in 10 CFR Part 50.54(q) were used as reference criteria.
b. Findings
No findings of significance were identified.
1EP5 Correction of Emergency Preparedness Weaknesses (71114.05 - One sample)
a. Inspection Scope
The inspectors reviewed a sampling of self-assessment procedures and reports to assess
NMPNS=s ability to evaluate their EP performance and programs. The inspectors reviewed a sampling of CRs from January 2007 through June 2008 initiated by NMPNS
concerning drills, self-assessments, and audits. Additionally, the inspectors reviewed:
EP Oversight Board meeting minutes; Qualit y and Performance Assurance reports; event reports for the September 2007 Alert and the May 2008 Unusual Event declarations at
NMPNS; and the 2007 50.54(t) audit report. The Planning Standard, 10 CFR Part
50.47(b)(14), and the related requirements of 10 CFR Part 50, Appendix E, were used as
reference criteria.
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation (71114.06 - One sample)
a. Inspection Scope
The inspectors observed control room operator emergency plan response actions during
the Unit 2 evaluated LORT scenario on September 5, 2008. The inspectors verified that
emergency classification declarations and notifications were completed in accordance with 18 10 CFR Part 50.72, 10 CFR Part 50 Appendix E, and the emergency implementing
procedures.
b. Findings
No findings of significance were identified.
RADIATION SAFETY
Cornerstone:
Occupational Radiation Safety 2OS1 Access Control to Radiologically Significant Areas (71121.01 - Six samples)
a. Inspection Scope
The inspectors reviewed radiation work permits for airborne radioactivity areas with the potential for individual worker internal exposures of greater than 50 millirem (mrem)
committed effective dose equivalent (20 derived air concentration (DAC)-hours). For
these selected airborne radioactive material areas, the inspectors verified barrier integrity
and engineering controls performance (e.g., high efficiency particulate air ventilation
system operation).
The inspectors reviewed and assessed the adequacy of NMPNS's internal dose
assessment for any actual internal exposur e greater than 50 mrem committed effective dose equivalent.
The inspectors examined NMPNS's physical and programmatic controls for highly
activated or contaminated materials (non-fuel) stored within the spent fuel pools.
The inspectors discussed with the acting radiation protection manager high dose rate-high
radiation area, and very high radiation area controls and procedures. The inspectors
focused on any procedural changes since the last inspection. The inspectors verified that
any changes to NMPNS's procedures did not substantially reduce the effectiveness and level of worker protection.
The inspectors discussed with health physics supervisors the controls in place for special
areas that have the potential to become very high radiation areas during certain plant
operations. The inspectors determined if these plant operations required communication
beforehand with the health physics group, so as to allow corresponding timely actions to
properly post and control the radiation hazards.
The inspectors verified adequate posting and locking of all entrances to high dose rate-
high radiation areas, and very high radiation areas.
The inspectors evaluated NMPNS's performance against the requirements contained in 10 CFR Part 20, Unit 1 TS 6.7, and Unit 2 TS 6.12.
b. Findings
No findings of significance were identified.
2OS2 ALARA Planning and Controls (71121.02 - Four samples)
a. Inspection Scope
The inspectors reviewed the results of the Spring 2008 Unit 2 refueling outage (2RFO11),
including the causes of any radiologically significant work (greater than five person-rem
collective exposure) which exceeded its dose estimate.
The inspectors obtained from NMPNS a list of wo rk activities ranked by actual/estimated exposure that are in progress or that have been completed during the last outage and
selected the two work activities of highest exposure significance.
The inspectors reviewed the as low as r easonably achievable (ALARA) work activity evaluations, exposure estimates, and exposure mitigation requirements. The inspectors
determined if NMPNS had established procedures, engineering and work controls, based on sound radiation protection principles to achieve occupational exposures that were ALARA. The inspectors determined if NMPNS had reasonably grouped the radiological
work into work activities, based on historic al precedence, industry norms, and/or special circumstances.
The inspectors compared the results achieved (dose rate reductions, person-rem used)
with the intended dose established in NMPNS's ALARA planning for these work activities.
The inspectors reviewed the assumptions and basis for the current annual collective
exposure estimate. The inspectors reviewed applicable procedures to determine the
methodology for estimating work activity-specific exposures and the intended dose outcome. The inspectors evaluated both dose rate and man-hour estimates for
reasonable accuracy.
The inspectors reviewed NMPNS's method for adjusting exposure estimates, or re-
planning work, when unexpected changes in scope or emergent work are encountered.
The inspectors determined if adjustments to estimated exposure (intended dose) were
based on sound radiation protection and ALARA principles or just adjusted to account for
failures to control the work.
The inspectors evaluated NMPNS's performance against the requirements contained in 10 CFR Part 20.1101.
b. Findings
No findings of significance were identified.
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - One sample)
a. Inspection Scope
The inspectors reviewed the plant UFSAR to identify applicable radiation monitors
associated with transient high and very high radiation areas including those used in
remote emergency assessment.
The inspectors evaluated NMPNS's performance against the requirements contained in 10
CFR Part 20.1501, 10 CFR Part 20.1703 and 10 CFR Part 20.1704.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151 - Seven samples)
a. Inspection Scope
The inspectors sampled NMPNS submittals fo r the performance indicators (PIs) listed below. To verify the accuracy of the PI data reported during that period, the PI definition
guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment
Performance Indicator Guideline," Revision 5, was used to verify the basis in reporting for
each data element.
Cornerstone:
The inspectors reviewed licensee event reports (LERs) and operator logs to determine
whether NMPNS accurately reported the number of unplanned power changes greater
than 20 percent at Unit 1 and Unit 2 from October 2007 to June 2008.
- Unit 1 unplanned power changes per 7000 critical hours
- Unit 2 unplanned power changes per 7000 critical hours
Cornerstone:
Unit 1 and Unit 2 LERs issued between the end of the third quarter 2007 and the end of
the second quarter 2008 were reviewed for safety system functional failures.
- Unit 1 safety system functional failures
- Unit 2 safety system functional failures 21 Cornerstone: Emergency Preparedness The inspectors reviewed data for the EP PIs which are: drill and exercise performance;
ERO Drill Participation; and ANS Reliability. The inspectors reviewed the PI data, its
supporting documentation, and the information NMPNS reported for the third and fourth
quarters of 2007, and the first and second quarters of 2008, to verify the accuracy of the
reported data. The acceptance criteria used for the review were 10 CFR Part 50.9 and
Additionally, the inspectors performed NRC Temporary Instruction (TI) 2515/175, ensured the completeness of NMPNS's completed Attachment 1 from the TI, and forwarded that
data to NRC Headquarters.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152 - Two samples)
.1 Review of Items Entered into the CAP
a. Inspection Scope
As specified by Inspection Procedure 71152, "Identification and Resolution of Problems,"
and in order to help identify repetitive equipment failures or specific human performance
issues for follow-up, the inspectors performed a daily screening of items entered into
NMPNS's CAP. In accordance with the baseline inspection procedures, the inspectors
also identified selected CAP items across t he initiating events, mitigating systems, and barrier integrity cornerstones for additional follow-up and review. The inspectors assessed
the threshold for problem identification, the adequacy of the cause analyses, extent of
condition review, operability determinations, and the timeliness of the specified corrective
actions.
b. Findings
No findings of significance were identified.
.2 Annual Sample - Review of Corrective Actions for Unit 1 Feedwater Heater Issues
a. Inspection Scope
This inspection focused on NMPNS's problem identification, evaluation, and resolution of
a Unit 1 level control valve (LCV)-26-09 actuator o-ring issue associated with the 122
FWH. On September 15, 2007, the 122 FWH tripped on high-high level when LCV-26-09
failed in the closed position and caused a cascading affect that backed up the water flow
to the other FWHs in the heater string. The 121 through 124 FWHs tripped due to high-
high level within 30 minutes, and the last FWH in the heater string (125) tripped several 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> later. This caused operators to reduce reactor power to less than 80 percent and
produced significant water-hammer in the FWH system piping. Following this event, operators initiated a condition report (CR 2007-5475) to resolve the issue. NMPNS
performed corrective maintenance on the valve actuator o-ring and repaired damaged
piping and supports on the 12 heater string prior to returning the system to service.
The inspectors selected the FWH issue for review because it resulted in an unplanned
reactivity change and power reduction, caused significant water-hammer in the system, and challenged plant operators. The inspectors reviewed NMPNS's associated
troubleshooting results, root cause evaluation, extent of condition review, and short-term and long-term corrective actions. The inspectors conducted a walkdown of accessible portions of the system, and reviewed the material condition of the LCVs, design control
measures, and configuration control. The inspectors also interviewed plant personnel and
reviewed procedures, related industry operating experience (OE), and the vendor manual
for the FWH LCV actuators. In addition, the inspectors reviewed the NMPNS TS and
UFSAR to ensure that NMPNS operated and maintained the FWH system as required.
b. Assessment and Observations
No findings of significance were identified. NMPNS used a failure modes and effects
analysis in the root cause evaluation to determine the nature of the LCV malfunction. The
root cause evaluation determined that the lubricant used in the actuator degraded to the
point where it caused the actuator o-rings to harden, thereby allowing air to leak past the
actuating piston. This caused insufficient air pressure to the valve actuator such that it
would not open the LCV on a demand signal. The inspectors determined that NMPNS
performed a thorough review of the issue and implemented appropriate corrective actions.
The corrective actions were aligned with the root cause analysis and included procedure
and preventive maintenance revisions, implement ing the use of a new lubricant, improved training to operators and engineering personnel on water-hammer mechanisms, and
operating experience program improvements.
The inspectors concluded that NMPNS had taken appropriate action in accordance with station procedures and the CAP. The
inspectors also determined that the root cause evaluation and subsequent follow-up
corrective maintenance were generally sufficient and based on the best available
information, troubleshooting, and relevant industry OE. In general, NMPNS's assigned
corrective actions were adequately tracked, appropriately documented, and completed as
scheduled.
.3 Annual Sample - Review of Corrective Actions for Inadvertent Carbon Dioxide (CO2)
Discharge
a. Inspection Scope
The inspectors reviewed NMPNS's evaluation and corrective actions associated with the
September 19, 2007 inadvertent discharge of CO2 from the fixed CO2 fire suppression system in the Unit 2 HPCS switchgear room (CR 2007-5538). The event occurred during
an installation of wiring in a local fire panel as part of a design change, and resulted in
NMPNS declaring an Alert at Unit 2. The inspectors reviewed NMPNS's root cause
analysis and corrective actions to ensure that appropriate evaluations were performed and 23 corrective actions were specified and prioritized. The inspectors also reviewed the follow-
up actions to verify that the root cause and corrective actions identified were addressed.
b. Findings
& Observations No findings of significance were identified. The inspectors determined that, in general, the
corrective actions taken associated with the inadvertent CO2 discharge were reasonable
and adequate.
4OA3 Followup of Events and Notices of Enforcement Discretion (71153 - Three samples)
.1 (Closed) LER 05000220/2008-001-00 , Loss of Offsite Power due to an Equipment
Malfunction On May 13, 2008, a loss of Unit 1 offsite power occurred due to an offsite equipment
failure which caused a loss of 115 kV offsite power line 4 while the remaining 115 kV
offsite power line (line 1) was removed from service for planned maintenance. The event
detailed in this LER was discussed in Section
4OA3 of Inspection Report
05000220/2008003. The inspectors reviewed this LER and no findings of significance
were identified. This LER is closed.
.2 (Closed) LER 05000410/2008-001-00 , Unqualified Relays Installed Since Original
Construction Result in an Unanalyzed Condition On April 10, 2008, NMPNS discovered that the J10 alarm relays in RB ventilation system
unit cooler motor starter circuits did not satisfy the environmental qualification
requirements of 10 CFR 50.49. This discovery came as a result of investigation of the
cause of J10 relay failures during loss of offsite power testing that was performed during
the 2008 refueling outage. J10 relay failures resulted in an NCV as documented in
Section 1R22 of Inspection Report 05000410/2008003. The inspectors reviewed this LER
and no additional findings of significance were identified. The failure of the J10 relays to
meet the environmental qualification requirements of 10 CFR 50.49 constitutes a violation
of minor significance that is not subject to enforcement action in accordance with Section
IV of the NRC Enforcement Policy. NMPNS entered the issues associated with this event into its CAP as CR 2008-2976. This LER is closed.
.3 Power Reduction due to a Maintenance-Related Electrical Transient
a. Inspection Scope
On July 14 at 1:12 p.m., Unit 2 experienced a partial loss of feedwater heating due to loss
of extraction steam to the 6B (high pressure) and 5C (low pressure) FWHs. The cause of
the event was an unrelated maintenance activity that unexpectedly produced an electrical
transient which affected a number of plant systems. Other consequences of the transient
were loss of the 'A' and 'C' heater drain pumps, loss of the 'B' offgas train, loss of normal
RB ventilation which resulted in automatic isolation of the RB and start of the standby gas
treatment system, and isolation of the hydrogen water chemistry system.
24 Operators responded in accordance with N2-SOP-08, "Unplanned Power Changes," and
N2-SOP-101D, "Rapid Power Reduction," to lower reactor power to 73 percent. After the
cause of the transient was identified, operators commenced recovery of the FWHs. While
attempting to restore the 5C FWH to service, resultant system perturbations caused an
isolation of the 6C FWH. With two high pressure FWHs (6B and 6C) out of service, N2-SOP-08 directed that an orderly plant shutdown be commenced. Operators resumed
power reduction until, at 50 percent power, the 6B FWH was successfully returned to
service. The plant shutdown was terminated and power ascension commenced in
coordination with restoration of the remaining affected systems. Power was restored to
full RTP on July 15.
The inspectors responded to the control room and observed operators' responses to the
event, and reviewed the circumstances surrounding the event.
b. Findings
Introduction.
A self-revealing Green finding was identified on July 14, 2008, when inadequate maintenance practices, during replacement and troubleshooting of a Unit 2
radioactive waste sump pump, caused an electrical transient that resulted in the loss of
numerous plant components and required a power reduction.
Description.
In May of 2008, radioactive waste sump pump 2DFW-P1A was replaced using a new model pump. The WO required that a rotation check be performed after the
electrical terminations had been completed. This, however, was not done because the
need for it was not recognized until after the pump had been installed in the sump.
Although work was stopped to determine a course of action, the pump remained available
for automatic operation as the backup sump pump. On July 8, 2008, it was recognized
that the pump had run several times since the work had been stopped, as indicated by the
pump run chart. This was incorrectly used to verify proper pump operation, and the
rotation check and PMT steps in the WO were signed off as complete.
On July 9, 2DFW-P1A was discovered to be running with no discharge pressure. In
developing a troubleshooting plan, NMPNS initial actions were to reverse power leads to
the pump. During testing the pump had no discharge pressure and, after two minutes, tripped on thermal overload. The leads were returned to the original configuration, and the pump was again energized by closing its circuit breaker on motor control center (MCC)
2NHS-MCC016. Shortly after the breaker was shut, noise was heard and flame was
observed coming from the breaker cubicle.
The feeder breaker from power board 2NSH-US9 to 2NHS-MCC016 tripped; however, the undervoltage transient to 2NSH-US9, caused by this failure (a short), resulted in the equipment losses discussed above.
In response to this event, the fire brigade responded to a fire alarm in the vicinity of 2NHS-
MCC016. They found no fire and observ ed the damaged breaker for 2DFW-P1A.
Operators responded to the partial loss of feedwater heating by reducing power to 73
percent. This issue was entered into the CAP as CR 2008-5745.
The cause of the event was that the pump suction and discharge were plugged with debris
from the sump, which resulted in high motor current due to the pump being in a bound 25 rotor condition. This, combined with a manufacturing defect associated with wiring
insulation in the breaker, resulted in a phase-to-ground short between the breaker and the
motor control center.
The performance deficiency associated with this event was inadequate maintenance
practices. Specifically: Following replacement in May, the pump was left in a condition
such that it would operate automatically pr ior to the performance of PMT; and, the PMT
was signed off based on pump run time rather than a verification of pump flow rate.
NMPNS procedure GAP-SAT-02, "Pre/Post-Maintenance Test Requirements," Revision
27, states that the PMT shall check components that were affected by the maintenance, verify that maintenance was properly performed, and verify that a new deficiency was not created. Had PMT been performed at the time of installation, low flow would likely have
shown that the pump discharge piping was already plugged with sump debris. This would
have prevented continued use of the pump and prevented subsequent troubleshooting
from focusing on the direction of motor rotation. Additionally: The troubleshooting plan
was inadequate in that, even if the pump had been rotating backwards, it would have
developed some discharge pressure; and, after the phase reversal had produced no
change in pump performance, the motor was restored to its original configuration and
tested, rather than to have reevaluated the troubleshooting plan. Constellation procedure
CNG-MN-1.01-1002, "Troubleshooting," Revision 0001, requires that troubleshooting shall
be stopped in the event of an unexpected equipment response, and that the
troubleshooting plan shall be reevaluated accordingly.
Analysis.
The finding was greater than minor because it was similar to IMC 0612, Appendix E, example 4.b, in that the inadequate maintenance resulted in a plant transient
that affected multiple systems and components. The finding affected the human
performance attribute of the Initiating Events cornerstone objective to limit the likelihood of
those events that upset plant stability and challenge critical safety functions during
shutdown as well as power operations. The finding was evaluated in accordance with IMC 0609, Attachment 4, and determined to be of very low safety significance (Green) per the
SDP Phase one determination because the finding did not contribute to both the likelihood
of a rector trip and the likelihood that mitigation equipment or functions would not be
available, and did not screen as potentially risk significant due to external events.
The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appropriately plan the pump troubl eshooting activity by incorporating abort criteria (H.3.a per IMC 0305).
Enforcement.
No violation of regulatory requirements occurred. The inspectors determined that the finding did not represent a noncompliance issue because it occurred on non safety-class balance of plant equipment. (FIN 05000410/2008004-02, Inadequate Maintenance Practices Result in a Plant Transient)26
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope
During the inspection period, the inspectors conducted observations of security force
personnel and activities to ensure that the ac tivities were consistent with NMPNS's security procedures and regulatory requirements relating to nuclear plant security. These
observations took place during both normal and off-normal plant working hours.
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an
integral part of the inspectors' normal plant status review and inspection activities.
b. Findings
No findings of significance were identified.
4OA6 Meetings, including Exit
Exit Meeting Summary
The inspectors presented the inspection results to Mr. Keith Polson and other members of
NMPNS management on October 24, 2008. NM PNS acknowledged that no proprietary information was involved.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- S. Belcher, Plant Manager
- W. Byrne, Manager, Nuclear Security
- R. Dean, Director, Quality and Performance Assessment
- J. Kaminski, Manager, Emergency Preparedness
- J. Krakuszeski, Manager, Operations
- J. Laughlin, Manager, Engineering Services
- K. Polson, Vice President
- J. Schultz, Chemistry Supervisor, J.A. FitzPatrick Nuclear Power Plant
- T. Shortell, Manager, Training
- S. Sova, Manager, Radiation Protection
- K. Stoffle, Environmental Support Supervisor
- J. Stone, Chemistry Technician
- T. Syrell, Director, Licensing
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
- 05000410/2008004-01 NCV Incorrect Risk Assessment for RCIC Unavailability (Section 1R13)
- 05000410/2008004-02 FIN Inadequate Maintenance Practices Result in
a Plant Transient (Section 4OA3)
Closed
- 05000220/LER-2008-001-00 LER Loss of Offsite Power due to an Equipment
- Malfunction (Section 4OA3)
- 05000410/LER-2008-001-00 LER Unqualified Relays Installed Since Original
- Construction Result in an Unanalyzed
- Condition (Section 4OA3)
Discussed
None.
Attachment
LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
- S-ODP-OPS-0112, "Offsite Power Operations and Interface," Revision 12
- N1-SOP-33A.3, "Major 115 KV Grid Disturbances," Revision 01
- N2-SOP-70, "Major Grid Disturbances," Revision 01
- EPIP-EPP-26, "Natural Hazard Preparation and Recovery," Revision 01
- N1-OP-64, "Meteorological Monitoring," Revision 01
- N2-OP-102, "Meteorological Monitoring," Revision 04
Section 1R04: Equipment Alignment
- N2-ELU-01, "Walkdown Order Electrical Lineup and Breaker Operations," Revision 00
- N1-OP-18, "Service Water System," Revision 02
- SDBD-502, "Service Water System Design Basis Document," Revision 07
- N1-ST-Q13, "Emergency Service Water Pump Operability Test," Revision 11
- N1-ST-V14, Service Water Check Valve And Emergency Service Water Pump and Check Valve Test," Revision 03
- N2-OP-33, "High Pressure Core Spray System," Revision 07
- N2-VLU-01, "Walkdown Order Valve Lineup and Valv
e Operations," Attachment 33, "N2-OP-33
- Walkdown Valve Lineup," Revision 00
- Piping and Instrumentation Diagram (P&ID)-33, "High Pressure Core Spray System"
Section 1R05: Fire Protection
- CMEB 9.5-1"
- NMPNS Unit 2 UFSAR, Appendix 9B, "Safe Shutdown Evaluation"
- N2-FPI-PFP-0201, "Unit 2 Pre-Fire Plans," Revision 0
Section 1R06: Flood Protection Measures
- Internal Flooding Analysis Notebook, Nine Mile Point Unit 1, Revision 00
- Nine Mile Point Nuclear Station - Unit 1 Individual Plant Examination, July 1993
- N1-PM-V-29, "Reactor Building Sump Pump System Operability Test," Revision 00
- CR 2006-5956
- ACR 06-06589
Section 1R07: Heat Sink Performance
- S15-79-HTX03, "Replacement Emergency Diesel Generator Raw Water Heat Exchanger Design," Revision 00
- S15-79-HTX-01, "Emergency Diesel Generator Cooling Water (EDGCW) Heat Exchanger Thermal Performance Evaluation," Revision 00, Disposition 00A
- Attachment
Section 1R11: Licensed Operator Requalification Program
- N1-SOP-32, "Generator Auxiliaries Failures," Revision 02
- N1-SOP-33A.1, "Loss of 115 KV," Revision 01
- N1-SOP-33A.3, "Major 115 KV Grid Disturbances," Revision 01
- N1-EOP-2, "RPV Control," Revision 01400
- N1-EOP-4, "Primary Containment Control," Revision 01400
- N2-SOP-60, "Loss of Drywell Cooling," Revision 04
- N2-SOP-03, "Loss of AC Power," Revision 08
- N2-SOP-06, "Feed Water Failures," Revision 04
- N2-SOP-101D, "Rapid Power Reduction," Revision 05
- N2-SOP-29, "Sudden Reduction in Core Flow," Revision 07
- N2-SOP-101C, "Reactor Scram," Revision 03
- N2-EOP-RPV, "RPV Control," Revision 11
- N2-EOP-PC, "Primary Containment Control," Revision 12
- N2-EOP-C4, "RPV Flooding," Revision 12
Section 1R12: Maintenance Effectiveness
- S-MRM-REL-0101, "Maintenance Rule," Revision 18
- S-MRM-REL-0104, "Maintenance Rule Scope," Revision 01
- S-MRM-REL-0105, "Maintenance Rule Performance Criteria," Revision 01
- Control Room HVAC System Health Reports, Q3-2006 through Q2-2008
- N2-TSP-HVC-R@001, "Testing and Analysis of Unit 2 Control Room Outdoor Air Special Filter Train System," Revision 01
- Reactor Recirculation System Health Reports, Q4-2007 through Q3-2008
- T-1792, "In-Place Testing of Nuclear Air Cleaning Systems for Nine Mile Point 2" Unit 2 Maintenance Rule Scoping Document
- ASCR 08-04282
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
- GAP-OPS-117, "Integrated Risk Management," Revision 14
- GAP-PSH-03, "Control of On-line Work Activities," Revision 15
- NAI-PSH-03, "On-line Work Management Process," Revision 11
Section 1R15: Operability Evaluations
- CNG-OP-1.01-1002, "Conduct of Operability Determinations / Functionality Assessments," Revision 00
- A10.1-N-341, "Revise SWP Pump IST Test Performance Flow Criteria from 9000 GPM to
- 10,000 GPM," Revision 00, Disposition 00H
- N2-OSP-SWP-@001, "SW Pump Curve Validation Test," Revision 04
- Attachment Section R18: Plant Modifications
- N1-MFT-105, "Replace CRD Timing Recorders," Revision 01
- C-22030-C, "Elementary Diagram Reactor Manual Control System," Sheet 1, Revision 33
- ESR 08-00812, "Raise 2SWP-TE-01 Setpoint to 150F for 2SWP*P1D"
- CFR Part 50.59 Applicability Determination Form for
- ESR 08-00812
- EC20080016-000, "Provide Alternate Power to the Main Step-Up Transformer 2MTX-XM1B
- Second Stage Cooling Pump and Fans," Revision 0000
- 08-15377-00, "Implement Temp Mod to Provide to Cooling Bank Two from Transformer 1D"
- CFR 50.59 Screening Form for EC20080016-000
Section 1R19: Post Maintenance Testing
- GAP-SAT-02, "Pre/Post Maintenance Test Requirements," Revision 26
- MDC-11, "Pump Curves and Acceptance Criteria," Revision 14
- S15-72-F003, "IST Approved Pump Curves Emergency Diesel Generator Cooling Water," Revision 08
- N1-MMP-079-119, "Diesel Generator Cooling Water Pumps Maintenance," Revision 02
- S-TTP-PUMP-@001, "Generic Pump Curve Validation Procedure," Revision 00
- N2-OSP-SWP-@001, "Service Water Pump Curve Validation Test," Revision 04
- A10.1-N-341, "Revise SWP Pump IST Test Performance Flow Criteria From 9,000 to 10,000
- GPM," Revision 00, Disposition 00H
- N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability Test - Division I
and II," Revision 05
- N2-OP-100B, "HPCS Diesel Generator," Revision 08
Section 1R22: Surveillance Testing
- CNG-HU-1.01, "Human Performance Program," Revision 01
- CNG-HU-1.01-1000, "Human Performance," Revision 02
- CNG-HU-1.01-1001, "Human Performance Tools and Verification Practices," Revision 02
- CNG-HU-1.01-1002, "Pre-Job Briefings and Post-Job Critiques," Revision 02
- GAP-SAT-01, "ST Program," Revision 16
- GAP-OPS-117, "Integrated Risk Management," Revision 14
Section 1EP2: Alert and Notification System Evaluation
- Wyle Research Report
- WR 82-26, "Qualification of the Oswego County Prompt Notification System for Nine Mile Point and James A. Fitzpatrick Nuclear Power Plants,"
- August 1982
- Wyle Research Report
- WR 84-22, "Evaluation of the Oswego County Prompt Notification System," June 1984
- Public Notification System Service Manual, Federal Signal Corporation Engineered Systems
- EPIP-EPP-30, "Prompt Notification System Problem Response," Revision 08
- EPMP-EPP-01, "Maintenance of Emergency Preparedness," Revision 24
- EPMP-EPP-08, "Maintenance, Testing and O
peration of the Oswego County Prompt Notification System," Revision 14
- All siren and tone alert radio CRs dated between July 2006 and June 2008
- Attachment
Section 1EP3: Emergency Response Organization Staffing and Augmentation System
- NMPNS Site Emergency Plan, Revision 54, Section 5, "Organization Control of Emergencies"
- EPIP-EPP-13, "Emergency Response Facilities Activation and Operation," Revision 19
- EPMP-EPP-01, "Maintenance of Emergency Preparedness," Revision 24
- EPMP-EPP-06, "Emergency Response Organization Notification Maintenance and Surveillance," Revision 15
- GAP-OPS-01, "Administration of Operations," Revision 49
- Nine Mile Point Emergency Response Organization Duty Roster, Revision 2008-11
- NMPNS Training Server Emergency Preparedness Job Matrices
- Report, "Nine Mile Point Off-Hours Un-Announced All-Report Drill," October 12, 2007
- CR 2008-5135
Section 1EP4: Emergency Action Level and Emergency Plan Changes
- NMPNS Site Emergency Plan, Revision 54
- Licensing Document Change Request S-06-SEP-004 for Emergency Plan Revision 54
- NRC Safety Evaluation for NMPNS Site Emergency Plan Revision 54
- EPMP-EPP-01, "Maintenance of Emergency Preparedness," Revision 24, Attachment 3, "10CFR50.54(Q) Evaluation and Effectiveness Review"
- CR 2007-7349
- 10CFR50.54(q) screenings and reviews, dated between August 2007 and June 2008
Section 1EP5: Correction of Emergency Preparedness Weaknesses
- CNG-QL-101-1004, "Quality Audit Process," Revision 01
- October 2007 Report of Audit
- EPP-07-01-N, Emergency Preparedness Program (10CFR50.54t Report) NMPNS Quality and Performance Assurance Assessment Reports:
- 07-037, "ERO Staffing"
- 07-054, "Observation of the June 7, 2007, EP Drill"
- 07-068, "Observation of the NRC Graded EP Exercise and Follow-up Activities"
- 08-005, "Use of Corrective Action Process in EP"
- 08-006, "EAL Review"
- 08-023, "Observation the of March 4, 2008, Drill"
- 08-058, "Technical Support Center Focus Area Drills"
- 08-064, "Observation of the June 26, 2008, Drill"
- EP Oversight Board Minutes (various dates)
- NMPNS Report for the September 19, 2007, Alert
- NMPNS Report for the May 13, 2008, Unusual Event
Condition Report
- Summary for all EP-related CRs dated between July 2007 and June 2008
Section 1EP6: Drill Evaluation
- EPIP-EPP-01, "Classification of Emergency Conditions at Unit 1," Revision 17
- EPIP-EPP-20, "Emergency Notifications," Revision 18
Section 2OS2: ALARA Planning and Controls
- NMP Unit 2 RFO11 Radiation Protection Post-Outage Report
Section 4OA1: Performance Indicator Verification
- EPMP-EPP-05, "Emergency Planning Program Self-Assessment," Revision 15
- Public Notification System PI data, July 2007 - June 2008
Section 4OA2: Identification and Resolution of Problems
- CNG-CM-1.01-1003, "Design Engineering and Configuration Control", Revision 00001
- N2-ARP-1, Revision 00, Attachment 29
- CNG-MN-1.01-1006, "Oversight of Supplemental Personnel," Revision 00200
- CNG-CM-1.01-2003, "Acceptance of Vendor Engineering Products," Revision 0000
- NIP-CON-01, "Design and Configuration Control Process," Revision 23
- Safety Manual Chapter 20, Attachment
- 4, "Electrical Safety Checklist"
- WO 07-02412-18
Condition Reports
- 2008-5827
- 2008-5692
- 2008-5824
- 2008-5738
- 2008-6947
- 2008-7083
- 2008-7092
- 2008-7222
- 2008-7172
- 2008-5028
- 2008-6946
- 2008-6879
- 2008-6894
- 2008-6787
- 2008-6674
- 2008-6330
- 2008-4021
- 2008-6400
- 2008-6468
- 2008-6588
- 2008-6513
- 2008-6834
- 2008-7259
- 2004-3751
- 2006-1498
- 2006-4548
- 2006-4845
- 2006-5063
- 2006-5133
- 2006-5523
- 2006-5758
- 2007-0359
- 2007-0542
- 2007-0552
- 2007-1179
- 2007-1198
- 2007-5411
- 2007-6783
- 2007-7070
- 2008-0126
- 2008-0253
- 2008-1678
- 2008-1698
- 2008-2208
- 2008-3501
- 2008-4031
- 2008-4422
- 2008-4453
- 2008-5449
- 2008-6946
- 2008-7365
LIST OF ACRONYMS
ADAMS Agency Documents
Access Management System
ESW emergency service water
F Fahrenheit
hr hour
IMC inspection manual chapter
kV kilovolt
MCC motor control center
mrem millirem
- LLC [[]]
A-8RPV reactor pressure vessel
WO work order
yr year