IR 05000354/2007002: Difference between revisions

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| issue date = 05/09/2007
| issue date = 05/09/2007
| title = IR 05000354-07-002, on 01/01/2007 - 03/31/2007; Hope Creek Generating Station; Resident Inspector Integrated Report
| title = IR 05000354-07-002, on 01/01/2007 - 03/31/2007; Hope Creek Generating Station; Resident Inspector Integrated Report
| author name = Burritt A L
| author name = Burritt A
| author affiliation = NRC/RGN-I/DRP/PB3
| author affiliation = NRC/RGN-I/DRP/PB3
| addressee name = Levis W
| addressee name = Levis W
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:May 9, 2007
[[Issue date::May 9, 2007]]


Mr. William LevisPresident and Chief Nuclear Officer PSEG LLC - N09 P. O. Box 236 Hancocks Bridge, NJ 08038
==SUBJECT:==
HOPE CREEK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000354/2007002


SUBJECT: HOPE CREEK GENERATING STATION - NRC INTEGRATED INSPECTIONREPORT 05000354/2007002
==Dear Mr. Levis:==
On March 31, 2007, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Hope Creek Generating Station. The enclosed integrated inspection report documents the inspection results, which were discussed on April 5, 2007, with Mr. George Barnes and other members of your staff.


==Dear Mr. Levis:==
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
On March 31, 2007, the US Nuclear Regulatory Commission (NRC) completed an inspection atyour Hope Creek Generating Station. The enclosed integrated inspection report documents the inspection results, which were discussed on April 5, 2007, with Mr. George Barnes and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, no findings of significance were identified. However,licensee-identified violations which were determined to be of very low safety significance are listed in this report. The NRC is treating these violations as non-cited violations (NCVs)
Based on the results of this inspection, no findings of significance were identified. However, licensee-identified violations which were determined to be of very low safety significance are listed in this report. The NRC is treating these violations as non-cited violations (NCVs)
consistent with Section VI.A.1 of the NRC Enforcement Policy because of the very low safety significance of the violations and because they are entered into your corrective action program.
consistent with Section VI.A.1 of the NRC Enforcement Policy because of the very low safety significance of the violations and because they are entered into your corrective action program.


If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Hope Creek Generating Station.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in the Mr. W. Levis2 2NRC Public Document Room or from the Publicly Available Records (PARS) component ofNRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Hope Creek Generating Station.


Sincerely,/RA/Arthur L. Burritt, ChiefProjects Branch 3 Division of Reactor ProjectsDocket No:50-354License No:NPF-57
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the


===Enclosure:===
Mr. NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Inspection Report 05000354/2007002


===w/Attachment:===
Sincerely,
Supplemental Informationcc w/encl:G. Barnes, Site Vice President D. Winchester, Vice President - Nuclear Assessments B. Clark, Director - Finance J. Perry, Hope Creek Plant Manager J. J. Keenan, General Solicitor, PSEG M. Wetterhahn, Esquire, Winston and Strawn, LLP Consumer Advocate, Office of Consumer Advocate, Commonwealth of Pennsylvania L. A. Peterson, Chief of Police and Emergency Management Coordinator P. Baldauf, Assistant Director of Radiation Protection Programs, State of New Jersey K. Tosch, Chief, Bureau of Nuclear Engineering, NJ Dept. of Environmental Protection
/RA/
Arthur L. Burritt, Chief Projects Branch 3 Division of Reactor Projects Docket No:
50-354 License No:
NPF-57 Enclosure:
Inspection Report 05000354/2007002 w/Attachment: Supplemental Information cc w/encl:
G. Barnes, Site Vice President D. Winchester, Vice President - Nuclear Assessments B. Clark, Director - Finance J. Perry, Hope Creek Plant Manager J. J. Keenan, General Solicitor, PSEG M. Wetterhahn, Esquire, Winston and Strawn, LLP Consumer Advocate, Office of Consumer Advocate, Commonwealth of Pennsylvania L. A. Peterson, Chief of Police and Emergency Management Coordinator P. Baldauf, Assistant Director of Radiation Protection Programs, State of New Jersey K. Tosch, Chief, Bureau of Nuclear Engineering, NJ Dept. of Environmental Protection H. Otto, Ph.D., Administrator, Interagency Programs, DNREC Division of Water Resources, State of Delaware N. Cohen, Coordinator - Unplug Salem Campaign E. Zobian, Coordinator - Jersey Shore Anti Nuclear Alliance


H. Otto, Ph.D., Administrator, Interagency Programs, DNREC Division of Water Resources, State of Delaware N. Cohen, Coordinator - Unplug Salem Campaign E. Zobian, Coordinator - Jersey Shore Anti Nuclear Alliance M
M


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000354/2007002; 01/01/2007 - 03/31/2007; Hope Creek Generating Station; ResidentInspector Integrated Report.The report covered a 13-week period of inspection by resident inspectors, regional healthphysicist inspectors, and regional reactor inspectors. No findings of significance were identified.
IR 05000354/2007002; 01/01/2007 - 03/31/2007; Hope Creek Generating Station; Resident
 
Inspector Integrated Report.
 
The report covered a 13-week period of inspection by resident inspectors, regional health physicist inspectors, and regional reactor inspectors. No findings of significance were identified.


The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.
The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.


===NRC-Identified and Self-Revealing Findings===
===NRC-Identified and Self-Revealing Findings===
No findings of significance were identified.
No findings of significance were identified.


===B.Licensee Identified Violations===
===Licensee Identified Violations===
Violations of very low safety significance, that were identified by Public Service EnterpriseGroup (PSEG) have been reviewed by the inspectors. Corrective actions taken or planned by PSEG have been entered into PSEG's corrective action program. These violations and corrective actions are listed in Section 4OA7 of this report.
Violations of very low safety significance, that were identified by Public Service Enterprise Group (PSEG) have been reviewed by the inspectors. Corrective actions taken or planned by PSEG have been entered into PSEG's corrective action program. These violations and corrective actions are listed in Section 4OA7 of this report.


=REPORT DETAILS=
=REPORT DETAILS=
Summary of Plant StatusThe Hope Creek Generating Station began the first quarter operating at 100% power. The plantwas shutdown on January 26, 2007, to cold shutdown conditions to execute a scheduled maintenance outage.During power ascension on January 29, 2007, Hope Creek automatically scrammed on lowreactor water level caused by a failed reactor feed pump minimum flow valve. The plant was returned to 100% power on February 2, 2007, and remained at or near full power for the remainder of the inspection period.1.REACTOR SAFETYCornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01)


====a. Inspection Scope====
===Summary of Plant Status===
(1 sample)The inspectors reviewed seasonal adverse weather preparation activities related to rivergrass intrusion conditions that impact the station service water system. Inspectors assessed implementation of PSEG's grassing readiness plan through plant walkdowns, corrective action program review, and discussions with cognizant managers and engineers. Documents reviewed by inspectors are listed in the attachment.
The Hope Creek Generating Station began the first quarter operating at 100% power. The plant was shutdown on January 26, 2007, to cold shutdown conditions to execute a scheduled maintenance outage.
 
During power ascension on January 29, 2007, Hope Creek automatically scrammed on low reactor water level caused by a failed reactor feed pump minimum flow valve. The plant was returned to 100% power on February 2, 2007, and remained at or near full power for the remainder of the inspection period.
 
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}}
 
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
a.
 
===Inspection Scope (1 sample)===
The inspectors reviewed seasonal adverse weather preparation activities related to river grass intrusion conditions that impact the station service water system. Inspectors assessed implementation of PSEGs grassing readiness plan through plant walkdowns, corrective action program review, and discussions with cognizant managers and engineers. Documents reviewed by inspectors are listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R04}}
{{a|1R04}}
 
==1R04 Equipment Alignment (71111.04).1Partial Walkdown (5 samples)==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}


===.1 Partial Walkdown (5 samples)===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial walkdowns of the following systems to verify theoperability of redundant or diverse trains and components when safety equipment was inoperable. The inspectors completed walkdowns to identify any discrepancies that could impact the function of the system, and therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control systems components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that PSEG had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program. Documents reviewed are listed in the attachment.
The inspectors performed partial walkdowns of the following systems to verify the operability of redundant or diverse trains and components when safety equipment was inoperable. The inspectors completed walkdowns to identify any discrepancies that could impact the function of the system, and therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control systems components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that PSEG had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program. Documents reviewed are listed in the attachment.


2Enclosure 'A' and 'C' 1E switchgear during planned maintenance on the 'B' 1E switchgear Redundant station service water (SSW) trains and support equipment duringmaintenance on the 'D' SSW pump and traveling water screen The 'A' & 'C' SSW trains, emergency diesel generators (EDGs), and 4KVswitchgear rooms during the emergent unavailability of the 'B' & 'D' SSW trains Redundant EDG, emergency core cooling systems (ECCS), SSW, filtration,recirculation, and ventilation system (FRVS), station auxiliary cooling system (SACS), and control room (CR) chilled water equipment during extended planned maintenance on the 'C' EDG and unplanned unavailability of the 'B' FRVS vent fan and 'A' CR chiller 'B' control room chilled water system after return to service following extendedplanned maintenance
C A and C 1E switchgear during planned maintenance on the B 1E switchgear C
Redundant station service water (SSW) trains and support equipment during maintenance on the D SSW pump and traveling water screen C
The A & C SSW trains, emergency diesel generators (EDGs), and 4KV switchgear rooms during the emergent unavailability of the B & D SSW trains C
Redundant EDG, emergency core cooling systems (ECCS), SSW, filtration, recirculation, and ventilation system (FRVS), station auxiliary cooling system (SACS), and control room (CR) chilled water equipment during extended planned maintenance on the C EDG and unplanned unavailability of the B FRVS vent fan and A CR chiller C
B control room chilled water system after return to service following extended planned maintenance


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R05}}
{{a|1R05}}
 
==1R05 Fire Protection (71111.05).1Fire Protection - Quarterly Tours==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
 
===.1 Fire Protection - Quarterly Tours===
a.
 
===Inspection Scope (10 samples)===
The inspectors conducted tours of ten areas to assess the material condition and operational status of fire protection features. The inspectors verified that combustible material and ignition sources were controlled in accordance with PSEGs administrative procedures; fire detection and suppression equipment was available for use; that passive fire barriers were maintained in good material condition; and that compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with PSEGs fire plan. The areas toured are listed below with their associated pre-fire plan designator. Other documents reviewed are listed in the attachment.


====a. Inspection Scope====
C FRH-II-571, diesel area heating, ventilation and air conditioning (HVAC)equipment room C
(10 samples)The inspectors conducted tours of ten areas to assess the material condition andoperational status of fire protection features. The inspectors verified that combustible material and ignition sources were controlled in accordance with PSEG's administrative procedures; fire detection and suppression equipment was available for use; that passive fire barriers were maintained in good material condition; and that compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with PSEG's fire plan. The areas toured are listed below with their associated pre-fire plan designator. Other documents reviewed are listed in the attachment.FRH-II-571, diesel area heating, ventilation and air conditioning (HVAC)equipment roomFRH-II-563, control area HVAC equipment roomsFRH-II-552, control room areaFRH-III-133, accessible turbine building rooms containing offsite power sourcebus ducts to safety-related 4KV bussesFRH-II-412, 'D' residual heat removal (RHR) pump and reactor core isolationcooling (RCIC) pump roomsFRH-II-531, Common EDG Corridor, 102' ElevationFRH-II-471, Refuel Floor, 201' ElevationFRH-II-424, Motor Control Center (MCC) Area, Room 4218, 77' ElevationFRH-II-431, MCC Area, Room 4303, 102' ElevationFRH-II-151, 'A' Recirc MG Set Room, 137' Elevation
FRH-II-563, control area HVAC equipment rooms C
FRH-II-552, control room area C
FRH-III-133, accessible turbine building rooms containing offsite power source bus ducts to safety-related 4KV busses C
FRH-II-412, D residual heat removal (RHR) pump and reactor core isolation cooling (RCIC) pump rooms C
FRH-II-531, Common EDG Corridor, 102' Elevation C
FRH-II-471, Refuel Floor, 201' Elevation C
FRH-II-424, Motor Control Center (MCC) Area, Room 4218, 77' Elevation C
FRH-II-431, MCC Area, Room 4303, 102' Elevation C
FRH-II-151, A Recirc MG Set Room, 137' Elevation


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R06}}
{{a|1R06}}
 
==1R06 Flood Protection Measures (71111.06).1Internal Flooding==
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06}}
 
===.1 Internal Flooding===
a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)The inspectors reviewed selected risk-important plant design features and PSEGprocedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors focused on mitigation strategies and equipment in the 'B' RHR pump room. The inspectors reviewed flood analysis and design documents, including the updated final safety analysis report, engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis. In addition, the inspectors walked down the 'B' RHR room and adjacent rooms in the reactor building to assess potential flooding vulnerabilities.
The inspectors reviewed selected risk-important plant design features and PSEG procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors focused on mitigation strategies and equipment in the B RHR pump room. The inspectors reviewed flood analysis and design documents, including the updated final safety analysis report, engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis. In addition, the inspectors walked down the B RHR room and adjacent rooms in the reactor building to assess potential flooding vulnerabilities.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R11}}
{{a|1R11}}
 
==1R11 Licensed Operator Requalification Program (71111.11).1Requalification Activities Review By Resident Staff==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
 
===.1 Requalification Activities Review By Resident Staff===
a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)The resident inspectors observed one annual licensed operator requalification simulatorexamination scenario on January 20, 2007, to assess operator performance and training effectiveness. The scenario involved a main turbine vibration problem, a failed reactor mode switch, and a steam leak in the turbine building. The inspectors assessed simulator fidelity and observed the simulator instructor's critique of operator performance.
The resident inspectors observed one annual licensed operator requalification simulator examination scenario on January 20, 2007, to assess operator performance and training effectiveness. The scenario involved a main turbine vibration problem, a failed reactor mode switch, and a steam leak in the turbine building. The inspectors assessed simulator fidelity and observed the simulator instructors critique of operator performance.


The inspectors also observed control room activities with emphasis on simulator identified areas for improvement. Finally, the inspectors reviewed applicable documents associated with licensed operator requalification as listed in the attachment.
The inspectors also observed control room activities with emphasis on simulator identified areas for improvement. Finally, the inspectors reviewed applicable documents associated with licensed operator requalification as listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R12}}
{{a|1R12}}
 
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
  (71111.12)
{{IP sample|IP=IP 71111.12}}
a.


====a. Inspection Scope====
===Inspection Scope (3 samples)===
(3 samples)4Enclosure The inspectors reviewed the three samples listed below for items such as:
The inspectors reviewed the three samples listed below for items such as:
: (1) appropriate work practices;
: (1) appropriate work practices;
: (2) identifying and addressing common cause failures; (3)scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR);
: (2) identifying and addressing common cause failures; (3)scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR);
Line 110: Line 161:
: (6) charging unavailability for performance;
: (6) charging unavailability for performance;
: (7) classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); and
: (7) classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); and
: (8) appropriateness of performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Documents reviewed are listed in the attachment. Items reviewed included the following:'A' RHR pump minimum flow valve failed to close;GS-HV-5029 reactor building to suppression chamber vacuum breaker isolationvalve slow closure; and'C' reactor auxiliaries cooling system (RACS) pump motor failure.
: (8) appropriateness of performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Documents reviewed are listed in the attachment. Items reviewed included the following:
C A RHR pump minimum flow valve failed to close; C
GS-HV-5029 reactor building to suppression chamber vacuum breaker isolation valve slow closure; and C
C reactor auxiliaries cooling system (RACS) pump motor failure.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R13}}
{{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
a.


====a. Inspection Scope====
===Inspection Scope (5 samples)===
(5 samples)The inspectors reviewed on-line risk management evaluations through direct observationand document reviews for the following configurations:Planned maintenance on the 'A' EDG on January 3, 2007;'B' 1E switchgear relay outage testing reclassified as online and performed onFebruary 8, 2007;Concurrent planned maintenance on the 'D' SSW pump, 'A' circulating waterpump, 'B' primary containment instrument gas compressor, and the 10K107 service air compressor on February 20-22, 2007;Unplanned unavailability of the 'B' FRVS vent fan and 'A' control room chillerduring planned extended maintenance on the 'C' EDG on March 7, 2007; andEmergent unavailability of the 'B' electro-hydraulic control (EHC) pump on March27 and 28, 2007.The inspectors reviewed the applicable risk evaluations, work schedules and controlroom logs for these configurations to verify that concurrent planned and emergent maintenance and test activities did not adversely affect the plant risk already incurred with these configurations. PSEG's risk management actions were reviewed during shift turnover meetings, control room tours, and plant walkdowns. The inspectors also used PSEG's on-line risk monitor (Equipment Out-Of-Service workstation) to gain insights into the risk associated with these plant configurations. Finally, the inspectors reviewed notifications documenting problems associated with risk assessments and emergent work evaluations. Documents reviewed are listed in the attachment.
The inspectors reviewed on-line risk management evaluations through direct observation and document reviews for the following configurations:
C Planned maintenance on the A EDG on January 3, 2007; C
B 1E switchgear relay outage testing reclassified as online and performed on February 8, 2007; C
Concurrent planned maintenance on the D SSW pump, A circulating water pump, B primary containment instrument gas compressor, and the 10K107 service air compressor on February 20-22, 2007; C
Unplanned unavailability of the B FRVS vent fan and A control room chiller during planned extended maintenance on the C EDG on March 7, 2007; and C
Emergent unavailability of the B electro-hydraulic control (EHC) pump on March 27 and 28, 2007.
 
The inspectors reviewed the applicable risk evaluations, work schedules and control room logs for these configurations to verify that concurrent planned and emergent maintenance and test activities did not adversely affect the plant risk already incurred with these configurations. PSEGs risk management actions were reviewed during shift turnover meetings, control room tours, and plant walkdowns. The inspectors also used PSEGs on-line risk monitor (Equipment Out-Of-Service workstation) to gain insights into the risk associated with these plant configurations. Finally, the inspectors reviewed notifications documenting problems associated with risk assessments and emergent work evaluations. Documents reviewed are listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R15}}
{{a|1R15}}
 
==1R15 Operability Evaluations==
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}
a.


====a. Inspection Scope====
===Inspection Scope (5 samples)===
(5 samples)The inspectors reviewed five operability determinations for degraded or non-conformingconditions associated with:SACS pipe support failure on December 20, 2006;Operation of the 6B feedwater heater with water level low-out-of-specification on December 31, 2006;'A' control room chiller temperature control valve inoperability on February 10, 2007;'B' SSW lube water supply system through-wall leakage on February 22 - 28,2007; and'B' FRVS vent fan unplanned inoperability on March 5, 2007.The inspectors reviewed the technical adequacy of the operability determinations toensure the conclusions were justified. The inspectors also walked down accessible equipment to corroborate the adequacy of PSEG's operability determinations.
The inspectors reviewed five operability determinations for degraded or non-conforming conditions associated with:
C SACS pipe support failure on December 20, 2006; C
Operation of the 6B feedwater heater with water level low-out-of-specification C
on December 31, 2006; C
A control room chiller temperature control valve inoperability on February 10, 2007; C
B SSW lube water supply system through-wall leakage on February 22 - 28, 2007; and C
B FRVS vent fan unplanned inoperability on March 5, 2007.
 
The inspectors reviewed the technical adequacy of the operability determinations to ensure the conclusions were justified. The inspectors also walked down accessible equipment to corroborate the adequacy of PSEGs operability determinations.


Additionally, the inspectors reviewed other PSEG identified safety-related equipment deficiencies during this report period and assessed the adequacy of their operability screenings. Notifications and documents reviewed are listed in the attachment.
Additionally, the inspectors reviewed other PSEG identified safety-related equipment deficiencies during this report period and assessed the adequacy of their operability screenings. Notifications and documents reviewed are listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R17}}
{{a|1R17}}
 
==1R17 Permanent Plant Modifications==
==1R17 Permanent Plant Modifications==
{{IP sample|IP=IP 71111.17}}
{{IP sample|IP=IP 71111.17}}
a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)The inspectors reviewed a design change associated with a valve (DA-HV-2097) in theservice water structure deicing line. The modification changed the controls of the motor operator on the valve such that the valve will be not open beyond 12% of full-open. The modification was installed to limit the amount of circulating water diverted from the cooling tower basin to the service water intake structure to minimize the chance of silt disturbance near the service water pump suctions.The design bases, licensing bases, modification instructions and post modification testingof the affected components were reviewed to verify the performance capability of this equipment was not adversely affected. The inspectors reviewed the applicable technical specifications for this equipment to ensure that operability requirements and allowable outage time limits were met. The inspectors also reviewed notifications documenting 6Enclosure deficiencies identified related to permanent plant modifications. The documentsreviewed as part of these inspections are listed in the attachment.
The inspectors reviewed a design change associated with a valve (DA-HV-2097) in the service water structure deicing line. The modification changed the controls of the motor operator on the valve such that the valve will be not open beyond 12% of full-open. The modification was installed to limit the amount of circulating water diverted from the cooling tower basin to the service water intake structure to minimize the chance of silt disturbance near the service water pump suctions.
 
The design bases, licensing bases, modification instructions and post modification testing of the affected components were reviewed to verify the performance capability of this equipment was not adversely affected. The inspectors reviewed the applicable technical specifications for this equipment to ensure that operability requirements and allowable outage time limits were met. The inspectors also reviewed notifications documenting deficiencies identified related to permanent plant modifications. The documents reviewed as part of these inspections are listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R19}}
{{a|1R19}}
 
==1R19 Post-Maintenance Testing (71111.19)==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}
a.
 
===Inspection Scope (6 samples)===
The inspectors reviewed the post-maintenance tests listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed test procedures to verify the procedure adequately tested the safety functions that may have been affected by the maintenance activity and the acceptance criteria in the procedure were consistent with the Updated Final Safety Analysis Report (UFSAR) and other design or license basis documentation. The inspectors also witnessed the test or reviewed the test data to verify test results adequately demonstrated restoration of the affected safety functions. Documents reviewed are listed in the attachment.


====a. Inspection Scope====
C WO 60056618, A emergency service water makeup valve design change
(6 samples)The inspectors reviewed the post-maintenance tests listed below to verify thatprocedures and test activities ensured system operability and functional capability. The inspectors reviewed test procedures to verify the procedure adequately tested the safety functions that may have been affected by the maintenance activity and the acceptance criteria in the procedure were consistent with the Updated Final Safety Analysis Report (UFSAR) and other design or license basis documentation. The inspectors also witnessed the test or reviewed the test data to verify test results adequately demonstrated restoration of the affected safety functions. Documents reviewed are listed in the attachment.WO 60056618, 'A' emergency service water makeup valve design change*WO 60065779, 'B' H2/O2 analyzer isolation valves bailey card replacement
* WO 60065779, B H2/O2 analyzer isolation valves bailey card replacement
*WO 30139614, replacement of the 'A' reactor recirculation pump seal package
* WO 30139614, replacement of the A reactor recirculation pump seal package
*WO 60066866, repair of steam leak on the 3A feedwater heater extraction steam piping*WO 60067170 and 60066955, repair of 'A' and 'C' drywell to suppressionchamber vacuum breaker indications*WO 60055819, 'C' EDG keepwarm pump replacementUltrasonic measurement data associated with the 3A feedwater heater extraction steampiping was reviewed by a NRC regional specialist. The repair methods and post-maintenance testing methodology was also reviewed by the regional specialist and determined to be adequate.
* WO 60066866, repair of steam leak on the 3A feedwater heater extraction steam piping
* WO 60067170 and 60066955, repair of A and C drywell to suppression chamber vacuum breaker indications
* WO 60055819, C EDG keepwarm pump replacement Ultrasonic measurement data associated with the 3A feedwater heater extraction steam piping was reviewed by a NRC regional specialist. The repair methods and post-maintenance testing methodology was also reviewed by the regional specialist and determined to be adequate.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R20}}
{{a|1R20}}
 
==1R20 Refueling and Other Outage Activities==
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20}}
{{IP sample|IP=IP 71111.20}}
.1Scheduled Maintenance Outage on January 26, 2007


====a. Inspection Scope====
===.1 Scheduled Maintenance Outage on January 26, 2007===
(1 sample)The plant was shutdown on January 26, 2007, to implement a planned maintenanceoutage. The primary purpose of the outage was to repair a steam leak on an extraction 7Enclosure steam line providing steam to the 3A feedwater heater and to replace the shaft sealpackage on the 'A' reactor recirculation pump. The inspectors reviewed these maintenance activities and they are documented in section 1R19, Post-Maintenance Testing.The inspectors reviewed PSEG's outage schedule and activities to verify that risk wasconsidered appropriately and that license and technical specification requirements were adhered to. The inspectors observed portions of the reactor shutdown and subsequent start up from the control room to verify PSEG adhered to station procedures and to evaluate operator performance. The inspectors toured areas of the plant that were normally inaccessible during power operations to verify that safety related and risk significant SSCs were maintained in an operable condition. The inspectors performed a walkdown of the drywell following completion of all maintenance activities to verify there was no evidence of system leakage and that debris had not been left behind that could affect performance of plant equipment. Documents reviewed are listed in the attachment.Hope Creek completed the scheduled maintenance outage on January 29, 2007, at10:51 pm when the main generator was synchronized to the 500 kV grid. At 11:10 pm the reactor protection system automatically inserted all control rods into the reactor core due to a reactor pressure vessel (RPV) water level control problem. The transient is described in more detail in section
a.
{{a|4OA3}}
 
==4OA3 , Event Followup.
===Inspection Scope (1 sample)===
The plant was shutdown on January 26, 2007, to implement a planned maintenance outage. The primary purpose of the outage was to repair a steam leak on an extraction steam line providing steam to the 3A feedwater heater and to replace the shaft seal package on the A reactor recirculation pump. The inspectors reviewed these maintenance activities and they are documented in section 1R19, Post-Maintenance Testing.
 
The inspectors reviewed PSEGs outage schedule and activities to verify that risk was considered appropriately and that license and technical specification requirements were adhered to. The inspectors observed portions of the reactor shutdown and subsequent start up from the control room to verify PSEG adhered to station procedures and to evaluate operator performance. The inspectors toured areas of the plant that were normally inaccessible during power operations to verify that safety related and risk significant SSCs were maintained in an operable condition. The inspectors performed a walkdown of the drywell following completion of all maintenance activities to verify there was no evidence of system leakage and that debris had not been left behind that could affect performance of plant equipment. Documents reviewed are listed in the attachment.
 
Hope Creek completed the scheduled maintenance outage on January 29, 2007, at 10:51 pm when the main generator was synchronized to the 500 kV grid. At 11:10 pm the reactor protection system automatically inserted all control rods into the reactor core due to a reactor pressure vessel (RPV) water level control problem. The transient is described in more detail in section 4OA3, Event Followup.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R22}}
{{a|1R22}}
 
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}
a.


====a. Inspection Scope====
===Inspection Scope (5 samples)===
(5 samples)The inspectors witnessed five surveillance tests and reviewed test data of selectedsurveillance tests listed below to verify that the test met the requirements of the Technical Specifications, UFSAR, and station procedures. The inspectors also determined whether the testing effectively demonstrated that the structures, systems, and components were operationally ready and capable of performing their intended safety functions. Documents reviewed are listed in the attachment.*WO 50099699, high pressure coolant injection (HPCI) system in-service test onJanuary 10, 2007*WO 50087561, 'B' emergency diesel generator 24 hour endurance test onJanuary 17, 2007*WO 50099736, quarterly 'B' & 'D' core spray pump in-service test on January 18, 2007*WO 50098995, control rod scram time surveillance on January 26, 2007
The inspectors witnessed five surveillance tests and reviewed test data of selected surveillance tests listed below to verify that the test met the requirements of the Technical Specifications, UFSAR, and station procedures. The inspectors also determined whether the testing effectively demonstrated that the structures, systems, and components were operationally ready and capable of performing their intended safety functions. Documents reviewed are listed in the attachment.
*WO 50101674, Class 1E, Channel D, 125 Volt Quarterly Battery Surveillance onMarch 21, 2007
* WO 50099699, high pressure coolant injection (HPCI) system in-service test on January 10, 2007
* WO 50087561, B emergency diesel generator 24 hour endurance test on January 17, 2007
* WO 50099736, quarterly B & D core spray pump in-service test on January 18, 2007
* WO 50098995, control rod scram time surveillance on January 26, 2007
* WO 50101674, Class 1E, Channel D, 125 Volt Quarterly Battery Surveillance on March 21, 2007


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1R23}}
{{a|1R23}}
 
==1R23 Temporary Plant Modifications (71111.23)==
==1R23 Temporary Plant Modifications==
{{IP sample|IP=IP 71111.23}}
a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)The inspectors reviewed a temporary plant modification (T-Mod 07-007) associated withthe 'A' control room chiller. The modification bypassed a thrust bearing high oil temperature switch that had failed and resulted in an unplanned trip of the chiller. The inspectors verified the modification was consistent with the design and licensing bases of the chilled water system and that the performance capability of the system was not degraded by the modification. The inspectors reviewed documents to verify PSEG followed their processes for implementing temporary modifications on plant SSCs. In addition, the inspectors verified the modified equipment alignment through control room instrumentation and plant walkdowns of accessible portions of the affected equipment.
The inspectors reviewed a temporary plant modification (T-Mod 07-007) associated with the A control room chiller. The modification bypassed a thrust bearing high oil temperature switch that had failed and resulted in an unplanned trip of the chiller. The inspectors verified the modification was consistent with the design and licensing bases of the chilled water system and that the performance capability of the system was not degraded by the modification. The inspectors reviewed documents to verify PSEG followed their processes for implementing temporary modifications on plant SSCs. In addition, the inspectors verified the modified equipment alignment through control room instrumentation and plant walkdowns of accessible portions of the affected equipment.


The inspectors also reviewed notifications documenting problems associated with equipment affected by temporary modifications. Documents reviewed are listed in the attachment.
The inspectors also reviewed notifications documenting problems associated with equipment affected by temporary modifications. Documents reviewed are listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.Cornerstone:  Emergency Preparedness (EP)1EP2Alert and Notification System (ANS) (71114.02)
No findings of significance were identified.


====a. Inspection Scope====
===Cornerstone: Emergency Preparedness (EP)===
(1 sample)An onsite review was conducted to assess the maintenance and testing of PSEG's ANS. During this inspection, the inspectors interviewed site EP staff responsible for implementation of the ANS testing and maintenance. Notifications pertaining to the ANS were reviewed for causes, trends, and corrective actions. The inspectors further discussed with PSEG the new ANS system design and its benefits over the previous system. The inspectors reviewed PSEG's original ANS design report to ensure compliance with those commitments for system maintenance and testing. The inspectors toured the Emergency Operations Facility (EOF). On March 28, 2007, the inspectors observed a silent test of the ANS. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.
{{a|1EP2}}
 
==1EP2 Alert and Notification System (ANS)==
{{IP sample|IP=IP 71114.02}}
a.
 
===Inspection Scope (1 sample)===
An onsite review was conducted to assess the maintenance and testing of PSEGs ANS.
 
During this inspection, the inspectors interviewed site EP staff responsible for implementation of the ANS testing and maintenance. Notifications pertaining to the ANS were reviewed for causes, trends, and corrective actions. The inspectors further discussed with PSEG the new ANS system design and its benefits over the previous system. The inspectors reviewed PSEGs original ANS design report to ensure compliance with those commitments for system maintenance and testing. The inspectors toured the Emergency Operations Facility (EOF). On March 28, 2007, the inspectors observed a silent test of the ANS. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|1EP3}}


9Enclosure
{{a|1EP3}}
==1EP3 Emergency Response Organization (ERO) Staffing and Augmentation System==
==1EP3 Emergency Response Organization (ERO) Staffing and Augmentation System==
{{IP sample|IP=IP 71114.03}}
{{IP sample|IP=IP 71114.03}}
a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)A review of Salem/Hope Creek's ERO augmentation staffing requirements and theprocess for notifying the ERO was conducted. This was performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation.
A review of Salem/Hope Creeks ERO augmentation staffing requirements and the process for notifying the ERO was conducted. This was performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation.


The inspectors reviewed procedures, notifications, and call-in drills associated with the ERO notification system and drills. The inspectors interviewed personnel responsible for testing the ERO augmentation process. The inspectors compared qualification requirements to the training records for a sample of ERO members. The inspectors also verified that the EP department staff were receiving required training as specified in the emergency plan. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.
The inspectors reviewed procedures, notifications, and call-in drills associated with the ERO notification system and drills. The inspectors interviewed personnel responsible for testing the ERO augmentation process. The inspectors compared qualification requirements to the training records for a sample of ERO members. The inspectors also verified that the EP department staff were receiving required training as specified in the emergency plan. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.


====b. Findings====
====b. Findings====
No findings of significance were identified.1EP4Emergency Action Level (EAL) and Emergency Plan Changes (71114.04)
No findings of significance were identified. {{a|1EP4}}
 
==1EP4 Emergency Action Level (EAL) and Emergency Plan Changes==
{{IP sample|IP=IP 71114.04}}
a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)Prior to this inspection, the NRC had received and acknowledged changes made to theSalem/Hope Creek Emergency Plan and implementing procedures. PSEG developed these changes in accordance with 10 CFR 50.54(q), and determined that the changes did not result in a decrease in effectiveness to the Plan. PSEG also determined that the plan continued to meet the requirements of 10 CFR 50.47(b) and 10 CFR 50 Appendix E.
Prior to this inspection, the NRC had received and acknowledged changes made to the Salem/Hope Creek Emergency Plan and implementing procedures. PSEG developed these changes in accordance with 10 CFR 50.54(q), and determined that the changes did not result in a decrease in effectiveness to the Plan. PSEG also determined that the plan continued to meet the requirements of 10 CFR 50.47(b) and 10 CFR 50 Appendix E.


During this inspection, the inspectors conducted a sampling review of Salem/Hope Creek's 10 CFR 50.54(q) screenings for the changes made to the Plan that could potentially result in a decrease in effectiveness. This review did not constitute NRC approval of the changes and, as such, the changes remain subject to future NRC inspection. Also, the NRC reviewed PSEG's EAL scheme for logic and consistency. The requirements in 10 CFR 50.54(q) were used as reference criteria.
During this inspection, the inspectors conducted a sampling review of Salem/Hope Creeks 10 CFR 50.54(q) screenings for the changes made to the Plan that could potentially result in a decrease in effectiveness. This review did not constitute NRC approval of the changes and, as such, the changes remain subject to future NRC inspection. Also, the NRC reviewed PSEGs EAL scheme for logic and consistency. The requirements in 10 CFR 50.54(q) were used as reference criteria.


====b. Findings====
====b. Findings====
No findings of significance were identified.1EP5Correction of Emergency Preparedness Weaknesses (71114.05)
No findings of significance were identified. {{a|1EP5}}
 
==1EP5 Correction of Emergency Preparedness Weaknesses==
{{IP sample|IP=IP 71114.05}}
a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)The inspectors reviewed EP self-assessments and audit reports to assess PSEG's abilityto evaluate their performance and programs. The inspectors reviewed notifications initiated from December, 2005 to March, 2007 at Salem/Hope Creek from drills, self-10Enclosure assessments, and audits. Applicable emergency planning standards of 10 CFR 50.47and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.
The inspectors reviewed EP self-assessments and audit reports to assess PSEGs ability to evaluate their performance and programs. The inspectors reviewed notifications initiated from December, 2005 to March, 2007 at Salem/Hope Creek from drills, self-assessments, and audits. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.


====b. Findings====
====b. Findings====
No findings of significance were identified.1EP6Drill Evaluation (71114.06)
No findings of significance were identified. {{a|1EP6}}


====a. Inspection Scope====
==1EP6 Drill Evaluation==
(1 sample)Resident inspectors evaluated the conduct of a simulator examination scenario onJanuary 20, 2007, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the simulated control room to verify that event classification and notifications were done in accordance with the Hope Creek Event Classification Guide. The inspectors also observed PSEG's critique of the examination to compare any inspector-observed weakness with those identified by PSEG personnel to verify whether PSEG was properly identifying weaknesses.
{{IP sample|IP=IP 71114.06}}
a.
 
===Inspection Scope (1 sample)===
Resident inspectors evaluated the conduct of a simulator examination scenario on January 20, 2007, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the simulated control room to verify that event classification and notifications were done in accordance with the Hope Creek Event Classification Guide. The inspectors also observed PSEGs critique of the examination to compare any inspector-observed weakness with those identified by PSEG personnel to verify whether PSEG was properly identifying weaknesses.


====b. Findings====
====b. Findings====
No findings of significance were identified.2.RADIATION SAFETYCornerstone:  Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (71121.01)
No findings of significance were identified.


====a. Inspection Scope====
==RADIATION SAFETY==
(7 samples)The inspectors reviewed all PSEG performance indicators for the Occupational RadiationSafety Cornerstone for followup.The inspectors identified exposure significant work areas within radiation areas, highradiation areas (<1 R/hr), or airborne radioactivity areas in the plant and reviewed associated PSEG controls and surveys of these areas to determine if controls (e.g.
===Cornerstone: Occupational Radiation Safety===
2OS1 Access Control to Radiologically Significant Areas (71121.01) a.
 
===Inspection Scope (7 samples)===
The inspectors reviewed all PSEG performance indicators for the Occupational Radiation Safety Cornerstone for followup.
 
The inspectors identified exposure significant work areas within radiation areas, high radiation areas (<1 R/hr), or airborne radioactivity areas in the plant and reviewed associated PSEG controls and surveys of these areas to determine if controls (e.g.
 
surveys, postings, barricades) were acceptable.
 
The inspectors walked down these areas or their perimeters to determine: whether prescribed radiation work permits, procedure, and engineering controls were in place, whether PSEG surveys and postings were complete and accurate, and whether air samplers were properly located.
 
The inspectors examined PSEGs physical and programmatic controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools.


surveys, postings, barricades) were acceptable.The inspectors walked down these areas or their perimeters to determine:  whetherprescribed radiation work permits, procedure, and engineering controls were in place, whether PSEG surveys and postings were complete and accurate, and whether air samplers were properly located.
The inspectors discussed with the Radiation Protection Manager high dose rate - high radiation areas, and very high radiation areas (VHRA) controls and procedures. The inspectors verified that any changes to PSEG procedures do not substantially reduce the effectiveness and level of worker protection.


11Enclosure The inspectors examined PSEG's physical and programmatic controls for highlyactivated or contaminated materials (non-fuel) stored within spent fuel and other storage
The inspectors discussed with first-line health physics supervisors the controls in place for special areas that have the potential to become VHRA during certain plant operations.


pools.The inspectors discussed with the Radiation Protection Manager high dose rate - highradiation areas, and very high radiation areas (VHRA) controls and procedures. The inspectors verified that any changes to PSEG procedures do not substantially reduce the effectiveness and level of worker protection.The inspectors discussed with first-line health physics supervisors the controls in placefor special areas that have the potential to become VHRA during certain plant operations.The inspectors reviewed and assessed the adequacy of PSEG's internal doseassessment for any actual internal exposure greater than 50 mrem committed effective dose equivalent (CEDE).
The inspectors reviewed and assessed the adequacy of PSEGs internal dose assessment for any actual internal exposure greater than 50 mrem committed effective dose equivalent (CEDE).


====b. Findings====
====b. Findings====
No findings of significance were identified.2OS2ALARA Planning and Controls (71121.02)
No findings of significance were identified.
 
2OS2 ALARA Planning and Controls (71121.02) a.
 
===Inspection Scope (2 samples)===
The inspectors reviewed the assumptions and basis for the current annual collective exposure estimate. The inspectors reviewed applicable procedures to determine the methodology for estimating work activity-specific exposures and the intended dose outcome.


====a. Inspection Scope====
The inspectors reviewed the exposure results and monitoring controls of declared pregnant workers. A total of six personnel were declared pregnant workers during 2006, with the maximum dose to an individual during the declaration period being 3 millirem.
(2 samples)The inspectors reviewed the assumptions and basis for the current annual collectiveexposure estimate. The inspectors reviewed applicable procedures to determine the methodology for estimating work activity-specific exposures and the intended dose outcome.The inspectors reviewed the exposure results and monitoring controls of declaredpregnant workers. A total of six personnel were declared pregnant workers during 2006, with the maximum dose to an individual during the declaration period being 3 millirem.


====b. Findings====
====b. Findings====
No findings of significance were identified.2OS3Radiation Monitoring Instrumentation and Protective Equipment (71121.03)
No findings of significance were identified.
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03)a.


====a. Inspection Scope====
===Inspection Scope (1 sample)===
(1 sample)The inspectors identified the types of portable radiation detection instrumentation usedfor job coverage of high radiation area work, other temporary area radiation monitors currently used in the plant, and continuous air monitors associated with jobs with the potential for workers to receive 50 mrem CEDE.
The inspectors identified the types of portable radiation detection instrumentation used for job coverage of high radiation area work, other temporary area radiation monitors currently used in the plant, and continuous air monitors associated with jobs with the potential for workers to receive 50 mrem CEDE.


====b. Findings====
====b. Findings====
12Enclosure No findings of significance were identified.4.OTHER ACTIVITIES4OA1Performance Indicator Verification (71151)
No findings of significance were identified.


====a. Inspection Scope====
==OTHER ACTIVITIES==
(6 samples)Cornerstone: Initiating EventsThe inspectors reviewed PSEG's program to gather, evaluate and report information onthe following performance indicators (PIs). The inspectors used the guidance contained in (Nuclear Energy Institute) NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 4, to assess the accuracy of PSEG's collection and reporting of PI data. The documents reviewed by the inspectors are listed in the attachment.Unplanned SCRAMS per 7,000 Critical HoursUnplanned SCRAMS with Loss of Normal Heat RemovalUnplanned Power Changes per 7,000 Critical HoursThe inspectors verified the accuracy and completeness of reported manual andautomatic unplanned scrams during the period of January 1, 2006 through December 31, 2006, for the "Unplanned Scrams per 7,000 Critical Hours" PI.The inspectors reviewed and verified PSEG's basis for including or excluding anyunplanned reactor scrams for the "Unplanned Scrams with Loss of Normal Heat Removal" PI during the period of January 1, 2006 through December 31, 2006.The inspectors verified the accuracy and completeness of reported transients thatresulted in unplanned changes in reactor power of greater than 20 percent power for the "Unplanned Power Changes per 7,000 Critical Hours" PI during the period of January 1, 2006 through December 31, 2006.Cornerstone: Emergency Preparedness (3 samples)Drill and Exercise PerformanceERO Drill ParticipationAlert and Notification System ReliabilityThe inspectors reviewed supporting documentation from EP drills and ANS tests duringthe period of January 1, 2006 through December 31, 2006 to verify the accuracy of the reported data.
{{a|4OA1}}
 
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
a.
 
===Inspection Scope (6 samples)===
===Cornerstone: Initiating Events===
The inspectors reviewed PSEGs program to gather, evaluate and report information on the following performance indicators (PIs). The inspectors used the guidance contained in (Nuclear Energy Institute) NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 4, to assess the accuracy of PSEGs collection and reporting of PI data. The documents reviewed by the inspectors are listed in the attachment.
 
C Unplanned SCRAMS per 7,000 Critical Hours C
Unplanned SCRAMS with Loss of Normal Heat Removal C
Unplanned Power Changes per 7,000 Critical Hours The inspectors verified the accuracy and completeness of reported manual and automatic unplanned scrams during the period of January 1, 2006 through December 31, 2006, for the Unplanned Scrams per 7,000 Critical Hours PI.
 
The inspectors reviewed and verified PSEGs basis for including or excluding any unplanned reactor scrams for the Unplanned Scrams with Loss of Normal Heat Removal PI during the period of January 1, 2006 through December 31, 2006.
 
The inspectors verified the accuracy and completeness of reported transients that resulted in unplanned changes in reactor power of greater than 20 percent power for the Unplanned Power Changes per 7,000 Critical Hours PI during the period of January 1, 2006 through December 31, 2006.
 
===Cornerstone: Emergency Preparedness (3 samples)===
C Drill and Exercise Performance C
ERO Drill Participation C
Alert and Notification System Reliability The inspectors reviewed supporting documentation from EP drills and ANS tests during the period of January 1, 2006 through December 31, 2006 to verify the accuracy of the reported data.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified. {{a|4OA2}}


13Enclosure
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
.1Review of Items Entered into the Corrective Action ProgramAs required by Inspection Procedure 71152, Identification and Resolution of Problems,and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into PSEG's corrective action program. This was accomplished by reviewing the description of each new notification and attending daily management review committee meetings.


Documents reviewed are listed in the attachment..2Annual Sample: Bailey Logic Module Failures
===.1 Review of Items Entered into the Corrective Action Program===
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into PSEG's corrective action program. This was accomplished by reviewing the description of each new notification and attending daily management review committee meetings.
 
Documents reviewed are listed in the attachment.


====a. Inspection Scope====
===.2 Annual Sample: Bailey Logic Module Failures===
(1 sample)The inspectors reviewed PSEG's actions to address an adverse trend in Bailey LogicModule failures. A number of issues have been identified in the PSEG corrective action program (CAP) describing a rising number of Bailey logic card failures. The issues were selected for review based on their potential to increase the likelihood of an initiating event or cause the inoperability of a safety system. The inspectors reviewed PSEG procedures, vendor documents, design change packages, notifications, orders, corrective actions, and apparent cause evaluations to understand the equipment functions and operational history, as well as the identification, evaluation, and corrective actions associated with the degraded conditions. System engineers, reactor operators and other PSEG staff were interviewed to gain additional insights on the failures.The following examples illustrate a sampling of issues associated with Bailey LogicModule failures:On August 25, 2006, a Bailey Logic Module failure resulted in automatic closure of aturbine auxiliaries cooling system (TACS) return isolation valve and an unplanned power reduction to 78% power. Operators manually isolated the 'B' SACS loop then restored TACS cooling to stabilize the plant. Post-event review identified that the Field Programmable Logic Array chip in the Bailey Logic Module failed causing the automatic isolation of the valve. Corrective actions included replacement of the failed logic card, failure analysis of the faulty card, and continuation of the Bailey card replacement project.On November 27, 2006, indication was lost for the 'D' emergency diesel generator outputbreaker. Operators ordered the emergent replacement of the card even though they suspected the problem only impacted the indication portion of the Bailey Logic Module.
a.
 
===Inspection Scope (1 sample)===
The inspectors reviewed PSEGs actions to address an adverse trend in Bailey Logic Module failures. A number of issues have been identified in the PSEG corrective action program (CAP) describing a rising number of Bailey logic card failures. The issues were selected for review based on their potential to increase the likelihood of an initiating event or cause the inoperability of a safety system. The inspectors reviewed PSEG procedures, vendor documents, design change packages, notifications, orders, corrective actions, and apparent cause evaluations to understand the equipment functions and operational history, as well as the identification, evaluation, and corrective actions associated with the degraded conditions. System engineers, reactor operators and other PSEG staff were interviewed to gain additional insights on the failures.
 
The following examples illustrate a sampling of issues associated with Bailey Logic Module failures:
On August 25, 2006, a Bailey Logic Module failure resulted in automatic closure of a turbine auxiliaries cooling system (TACS) return isolation valve and an unplanned power reduction to 78% power. Operators manually isolated the B SACS loop then restored TACS cooling to stabilize the plant. Post-event review identified that the Field Programmable Logic Array chip in the Bailey Logic Module failed causing the automatic isolation of the valve. Corrective actions included replacement of the failed logic card, failure analysis of the faulty card, and continuation of the Bailey card replacement project.
 
On November 27, 2006, indication was lost for the D emergency diesel generator output breaker. Operators ordered the emergent replacement of the card even though they suspected the problem only impacted the indication portion of the Bailey Logic Module.


The post-replacement testing revealed that the failure would have prevented automatic and main control room operation of the diesel output breaker. Corrective actions included replacement of the failed logic card, a more detailed failure analysis of the faulty card, and re-evaluation of the Bailey card replacement project.
The post-replacement testing revealed that the failure would have prevented automatic and main control room operation of the diesel output breaker. Corrective actions included replacement of the failed logic card, a more detailed failure analysis of the faulty card, and re-evaluation of the Bailey card replacement project.


====b. Findings====
====b. Findings====
& Observations 14Enclosure No findings of significance were identified.The inspectors found that PSEG appropriately identified degraded conditions associatedwith Bailey Logic Module failures and entered them into the corrective action program.
& Observations No findings of significance were identified.
 
The inspectors found that PSEG appropriately identified degraded conditions associated with Bailey Logic Module failures and entered them into the corrective action program.
 
Evaluations of degraded conditions were thorough, and included considerations for extent of condition. The inspectors reviewed the above examples and determined that performance deficiencies did not exist. Corrective actions developed by PSEG were appropriate to adequately address identified deficiencies.
{{a|4OA3}}
 
==4OA3 Event Followup==
{{IP sample|IP=IP 71153}}
 
===.1 Hope Creek Automatic Scram on January 29, 2007===
a.
 
===Inspection Scope (1 sample)===
Hope Creek completed a scheduled maintenance outage on January 29, 2007, at 10:51 pm when the main generator was synchronized to the 500 kV grid. At 11:02 pm, control room operators observed reactor water level lower than expected and took action to restore level. Efforts to restore reactor water level were unsuccessful. At 11:10 pm, RPV water level was below 12.5 inches and the reactor protection system automatically inserted all control rods into the reactor core (a reactor scram).


Evaluations of degraded conditions were thorough, and included considerations for extent of condition. The inspectors reviewed the above examples and determined that performance deficiencies did not exist. Corrective actions developed by PSEG were appropriate to adequately address identified deficiencies.4OA3Event Followup (71153).1Hope Creek Automatic Scram on January 29, 2007
The inspectors responded to the control room following the reactor scram to observe post-scram operations. The inspectors collected data from the plant computer to evaluate plant conditions prior to, during, and following the transient. The inspectors observed and participated in interviews with control room operators to gain an understanding of how operators responded to the transient. The inspectors observed engineering technical analysis and evaluation meetings and interviewed engineers to gain an understanding of the transient and to assess PSEGs evaluation process. The inspectors observed the Plant Oversight Review Committee meeting prior to plant startup to evaluate whether PSEG appropriately resolved the issues that led to the transient.


====a. Inspection Scope====
A root cause evaluation identified a failed reactor feed pump minimum flow valve as the cause of the level control problem and subsequent reactor scram. Corrective actions included repair of a reactor feed pump flow instrument tubing line and clarification to the low power operating portion of the feedwater system operating procedure. Documents reviewed are listed in the attachment.
(1 sample)Hope Creek completed a scheduled maintenance outage on January 29, 2007, at 10:51pm when the main generator was synchronized to the 500 kV grid. At 11:02 pm, control room operators observed reactor water level lower than expected and took action to restore level. Efforts to restore reactor water level were unsuccessful. At 11:10 pm, RPV water level was below 12.5 inches and the reactor protection system automatically inserted all control rods into the reactor core (a reactor scram).The inspectors responded to the control room following the reactor scram to observepost-scram operations. The inspectors collected data from the plant computer to evaluate plant conditions prior to, during, and following the transient. The inspectors observed and participated in interviews with control room operators to gain an understanding of how operators responded to the transient. The inspectors observed engineering technical analysis and evaluation meetings and interviewed engineers to gain an understanding of the transient and to assess PSEG's evaluation process. The inspectors observed the Plant Oversight Review Committee meeting prior to plant startup to evaluate whether PSEG appropriately resolved the issues that led to the transient.A root cause evaluation identified a failed reactor feed pump minimum flow valve as thecause of the level control problem and subsequent reactor scram. Corrective actions included repair of a reactor feed pump flow instrument tubing line and clarification to the low power operating portion of the feedwater system operating procedure. Documents reviewed are listed in the attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified..2(Closed) LER 05000354/2006-005-00, Drywell Hoist Breaker Not Open Prior to Mode 2EntryOn December 18, 2006, PSEG identified that breaker 52-263042 for the drywell safetyrelief valve (SRV) hoist was in the closed position. Technical Specification 3.8.4.1 15Enclosure requires that breaker 52-263042 be administratively maintained open in OperationalCondition 1, 2, and 3. The breaker was not open and administratively controlled prior to entry into Operating Condition 2 on May 2, 2006. The inspectors reviewed the licensee event report (LER) and evaluations associated with the performance deficiency. The enforcement aspects of this finding are discussed in Section
No findings of significance were identified.
{{a|4OA7}}
 
==4OA7 . This LER is closed.4OA5Other Activities.1Independent Spent Fuel Storage Installation (ISFSI)==
===.2 (Closed) LER 05000354/2006-005-00, Drywell Hoist Breaker Not Open Prior to Mode 2===
Entry On December 18, 2006, PSEG identified that breaker 52-263042 for the drywell safety relief valve (SRV) hoist was in the closed position. Technical Specification 3.8.4.1 requires that breaker 52-263042 be administratively maintained open in Operational Condition 1, 2, and 3. The breaker was not open and administratively controlled prior to entry into Operating Condition 2 on May 2, 2006. The inspectors reviewed the licensee event report (LER) and evaluations associated with the performance deficiency. The enforcement aspects of this finding are discussed in Section 4OA7. This LER is closed.
 
{{a|4OA5}}
 
==4OA5 Other Activities==
===.1 Independent Spent Fuel Storage Installation (ISFSI)===
{{IP sample|IP=IP 60855}}
{{IP sample|IP=IP 60855}}
a.
===Inspection Scope (1 sample)===
The inspection was a follow-up to Inspection Report 05000354/2006010, completed on November 9, 2006. This inspection consisted of evaluating post dry cask storage activities associated with the recent completion of Hope Creeks initial ISFSI fuel loading campaign. Inspection activities consisted of interviews with cognizant personnel and reviews of PSEG documentation. Areas inspected included review of final dose totals for the initial ISFSI campaign, completed work packages, effectiveness of corrective actions implemented after loading of the first canister, PSEG identified lessons-learned during the initial campaign, ISFSI-related notifications, and verification of personnel training and qualifications.
The inspectors reviewed the completed work package for the loading of the first canister.
The work package included the procedures for loading and sealing the multi purpose canister (MPC), weld data sheets, liquid penetrant examination reports, and daily polar crane check lists. The inspectors verified that procedure steps were completed and necessary signatures and approvals obtained as required.
The inspectors interviewed cognizant personnel regarding the meaning and purpose of various signature completion steps in procedure NC.MD-PM.DCS-0003, Sealing, Drying, and Backfilling of a Loaded MPC. PSEG personnel confirmed that signatures for various steps signified that work was successfully completed and that associated data sheets had been reviewed by qualified individuals.


====a. Inspection Scope====
The inspectors discussed the training and qualification requirements for the Cask Loading Supervisor position with cognizant personnel. The inspectors determined that designated individuals were qualified as Cask Loading Supervisors in accordance with PSEGs program to meet the requirements of ANSI/ANS-3.1-1981, section 4.3.2. In addition these individuals were required to attend various training classes that included such topics as contract management, supplemental personnel oversight, and QA orientation. The inspectors observed that PSEG formally documented that individuals were properly qualified per ANSI/ANS-3.1, verified that the training database contained the documentation in the records for three individuals designated as Cask Loading Supervisors, and verified the required training for these individuals was maintained current.
(1 sample)The inspection was a follow-up to Inspection Report 05000354/2006010, completed onNovember 9, 2006. This inspection consisted of evaluating post dry cask storage activities associated with the recent completion of Hope Creek's initial ISFSI fuel loading campaign. Inspection activities consisted of interviews with cognizant personnel and reviews of PSEG documentation. Areas inspected included review of final dose totals for the initial ISFSI campaign, completed work packages, effectiveness of corrective actions implemented after loading of the first canister, PSEG identified lessons-learned during the initial campaign, ISFSI-related notifications, and verification of personnel training and qualifications.The inspectors reviewed the completed work package for the loading of the first canister. The work package included the procedures for loading and sealing the multi purpose canister (MPC), weld data sheets, liquid penetrant examination reports, and daily polar crane check lists. The inspectors verified that procedure steps were completed and necessary signatures and approvals obtained as required.The inspectors interviewed cognizant personnel regarding the meaning and purpose ofvarious signature completion steps in procedure NC.MD-PM.DCS-0003, "Sealing, Drying, and Backfilling of a Loaded MPC."  PSEG personnel confirmed that signatures for various steps signified that work was successfully completed and that associated data sheets had been reviewed by qualified individuals. The inspectors discussed the training and qualification requirements for the CaskLoading Supervisor position with cognizant personnel. The inspectors determined that designated individuals were qualified as Cask Loading Supervisors in accordance with PSEG's program to meet the requirements of ANSI/ANS-3.1-1981, section 4.3.2. In addition these individuals were required to attend various training classes that includedsuch topics as contract management, supplemental personnel oversight, and QA orientation. The inspectors observed that PSEG formally documented that individuals were properly qualified per ANSI/ANS-3.1, verified that the training database contained the documentation in the records for three individuals designated as Cask Loading Supervisors, and verified the required training for these individuals was maintained current.
 
The inspectors reviewed PSEG actions in response to exceeding the first fuel campaign dose estimate by approximately 1.5 rem. PSEG conducted a post-job critique after the first loading.


16Enclosure The inspectors reviewed PSEG actions in response to exceeding the first fuel campaigndose estimate by approximately 1.5 rem. PSEG conducted a post-job critique after the first loading.The inspectors reviewed PSEG's ISFSI-related corrective action notifications, lessons-learned documentation and action plans. Areas identified for evaluation included polarcrane reliability improvements, dose reduction efforts, and transporter maintenance.
The inspectors reviewed PSEGs ISFSI-related corrective action notifications, lessons-learned documentation and action plans. Areas identified for evaluation included polar crane reliability improvements, dose reduction efforts, and transporter maintenance.


====b. Findings====
====b. Findings====
No findings of significance were identified..2(Closed) URI 05000354/2006015-03, Inspection of PRA Quality Issues, and NRC Reviewof Human Error Probability (HEP) Assigned Value for Battery Charger Cross-tie OperatorActionThe Senior Reactor Analyst (SRA) reviewed the unresolved item (URI) crediting operatoraction, NR-XTIE-CHARGE, in PSEG's probabilistic risk assessment (PRA) to determine if the model was reasonably representative of the as-built, as-operated nuclear power unit which it represents. This action is credited during postulated loss-of-offsite power (LOOP) events with an assumed concurrent failure of the 'B' and 'D' EDGs. Specifically, the Hope Creek PRA model credits manual operator actions to cross-tie power to the 'B' or 'D' battery chargers to provide power to the SRVs for reactor pressure control. For the NR-XTIE-CHARGE action to be successful, it must be completed prior to the depletion of the batteries. During the Component Design Bases Inspection, completed on December 7, 2006, the inspection team questioned the appropriateness of assigning a HEP of 0.6 when the performance shaping factors, such as training, availability of equipment and diagnosis were not favorable. An inappropriate assignment of an HEP could have an adverse impact on the ability of PSEG to assess and manage risk during normal plant operations.The SRA conducted a sensitivity analysis for maintenance rule risk assessments whichwould be impacted by the NR-XTIE-CHARGE operator action. The most limiting maintenance configuration would be a HPCI system unavailability with 'B' SACS in standby, 'D' SSW pump in standby, 'B' control rod drive pump in standby, and air compressor 10K107 in standby. A bounding unavailability of 14 days was assigned, which is the technical specification allowed outage time for HPCI. This was consideredconservative because the 2002 - 2004 unavailability data from the Mitigating System Performance Index (MSPI) bases documents shows that the largest HPCI unavailability for this period occurred in July 2004 in which 154.23 hrs. (6.43 days). There were no significant outages of other monitored components during this period. Other MSPI components included in the sensitivity analysis were also reviewed and found to have a negligible impact. The HEP evaluated for the analysis ranged from PSEG's assigned value of 0.6 (60% chance of failure) to 1.0 (100% chance of failure). Utilizing the guidance provided in Inspection Manual Chapter (IMC) 0609, Appendix K, "Maintenance Risk Assessment and Risk Management Significance Determination Process," the SRA concluded that under the most bounding assumptions, the changes in the maintenance 17Enclosure rule risk assessment would not be significant and would be within the acceptable rangeof PRA uncertainty.The generic issues associated with PRA quality are being addressed by the staff asoutlined and updated in SECY-07-0042, "Status of the Plan for the Implementation of the Commission's Phased Approach to Probabilistic Risk Assessment Quality," issued on March 7, 2007. The SRA concluded that the sensitivity of NR-XTIE-CHARGE did not impact the ability of PSEG to assess and manage risk during normal plant operations.
No findings of significance were identified.
 
===.2 (Closed) URI 05000354/2006015-03, Inspection of PRA Quality Issues, and NRC Review===
of Human Error Probability (HEP) Assigned Value for Battery Charger Cross-tie Operator Action The Senior Reactor Analyst (SRA) reviewed the unresolved item (URI) crediting operator action, NR-XTIE-CHARGE, in PSEGs probabilistic risk assessment (PRA) to determine if the model was reasonably representative of the as-built, as-operated nuclear power unit which it represents. This action is credited during postulated loss-of-offsite power (LOOP) events with an assumed concurrent failure of the B and D EDGs. Specifically, the Hope Creek PRA model credits manual operator actions to cross-tie power to the B or D battery chargers to provide power to the SRVs for reactor pressure control. For the NR-XTIE-CHARGE action to be successful, it must be completed prior to the depletion of the batteries. During the Component Design Bases Inspection, completed on December 7, 2006, the inspection team questioned the appropriateness of assigning a HEP of 0.6 when the performance shaping factors, such as training, availability of equipment and diagnosis were not favorable. An inappropriate assignment of an HEP could have an adverse impact on the ability of PSEG to assess and manage risk during normal plant operations.
 
The SRA conducted a sensitivity analysis for maintenance rule risk assessments which would be impacted by the NR-XTIE-CHARGE operator action. The most limiting maintenance configuration would be a HPCI system unavailability with B SACS in standby, D SSW pump in standby, B control rod drive pump in standby, and air compressor 10K107 in standby. A bounding unavailability of 14 days was assigned, which is the technical specification allowed outage time for HPCI. This was considered conservative because the 2002 - 2004 unavailability data from the Mitigating System Performance Index (MSPI) bases documents shows that the largest HPCI unavailability for this period occurred in July 2004 in which 154.23 hrs. (6.43 days). There were no significant outages of other monitored components during this period. Other MSPI components included in the sensitivity analysis were also reviewed and found to have a negligible impact. The HEP evaluated for the analysis ranged from PSEGs assigned value of 0.6 (60% chance of failure) to 1.0 (100% chance of failure). Utilizing the guidance provided in Inspection Manual Chapter (IMC) 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, the SRA concluded that under the most bounding assumptions, the changes in the maintenance rule risk assessment would not be significant and would be within the acceptable range of PRA uncertainty.


As such, for this issue it was determined that the model was reasonably representative of the as-built, as-operated nuclear power unit which it represents and this URI is closed.4OA6Meetings, Including ExitOn April 5, 2007, the inspectors presented their findings to members of PSEG management led by Messrs. Barnes and Perry. None of the information reviewed by the inspectors was considered proprietary. 4OA7Licensee-Identified ViolationsThe following violations of very low safety significance (Green) were identified by PSEGand are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as Non-Cited Violations.Technical Specification 6.12.1 requires that access to, and activities in, each highradiation area be controlled by means of a radiation work permit. Entry into such areas shall be made only after dose rates in the area have been determined and entry personnel are knowledgeable of them. On December 12, 2006, a mechanical maintenance technician ascended into the Unit 1 turbine building crane cab, a posted high radiation area, without having been briefed or signed in on the appropriate high radiation area radiation work permit. The event is documented in PSEG's CAP as notification 20306791. The finding is only of very low safety significance because it did not involve a very high radiation area or personnel over-exposure.Technical Specification 3.8.4.1, "Primary Containment Penetration ConductorOvercurrent Protective Devices," requires that breaker 52-263042 for the drywell SRV hoist be administratively maintained open in Operational Conditions 1, 2, and 3. Contrary to this requirement, on December 18, 2006, PSEG identified that this breaker was closed. PSEG entered this issue into their corrective action program as notification 20307894. It was subsequently determined that the breaker had been closed since Hope Creek entered Operating Condition 2 on May 2, 2006. The issue was determined to be of very low safety significance, based on IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, because the finding does not represent an actual open pathway in the physical integrity of reactor containment.
The generic issues associated with PRA quality are being addressed by the staff as outlined and updated in SECY-07-0042, Status of the Plan for the Implementation of the Commissions Phased Approach to Probabilistic Risk Assessment Quality, issued on March 7, 2007. The SRA concluded that the sensitivity of NR-XTIE-CHARGE did not impact the ability of PSEG to assess and manage risk during normal plant operations.


18Enclosure ATTACHMENT:
As such, for this issue it was determined that the model was reasonably representative of the as-built, as-operated nuclear power unit which it represents and this URI is closed.
 
{{a|4OA6}}
 
==4OA6 Meetings, Including Exit==
On April 5, 2007, the inspectors presented their findings to members of PSEG management led by Messrs. Barnes and Perry. None of the information reviewed by the inspectors was considered proprietary.
 
{{a|4OA7}}
 
==4OA7 Licensee-Identified Violations==
The following violations of very low safety significance (Green) were identified by PSEG and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as Non-Cited Violations.
 
C Technical Specification 6.12.1 requires that access to, and activities in, each high radiation area be controlled by means of a radiation work permit. Entry into such areas shall be made only after dose rates in the area have been determined and entry personnel are knowledgeable of them. On December 12, 2006, a mechanical maintenance technician ascended into the Unit 1 turbine building crane cab, a posted high radiation area, without having been briefed or signed in on the appropriate high radiation area radiation work permit. The event is documented in PSEGs CAP as notification 20306791. The finding is only of very low safety significance because it did not involve a very high radiation area or personnel over-exposure.
 
C Technical Specification 3.8.4.1, "Primary Containment Penetration Conductor Overcurrent Protective Devices," requires that breaker 52-263042 for the drywell SRV hoist be administratively maintained open in Operational Conditions 1, 2, and 3. Contrary to this requirement, on December 18, 2006, PSEG identified that this breaker was closed. PSEG entered this issue into their corrective action program as notification 20307894. It was subsequently determined that the breaker had been closed since Hope Creek entered Operating Condition 2 on May 2, 2006. The issue was determined to be of very low safety significance, based on IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, because the finding does not represent an actual open pathway in the physical integrity of reactor containment.
 
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
===Licensee personnel===
===Licensee personnel===
: [[contact::G. Barnes]], Station Vice President
: [[contact::G. Barnes]], Station Vice President
Line 320: Line 527:
: [[contact::J. Harris]], ALARA Engineer
: [[contact::J. Harris]], ALARA Engineer
: [[contact::F. Foster]], Operations Maintenance and Technical Instructor
: [[contact::F. Foster]], Operations Maintenance and Technical Instructor
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
Opened NoneOpened/Closed05000354/2006-005-00LER Drywell Hoist Breaker Not Open Prior to Mode 2Entry (Section 4OA3.2)
===Opened===
None
 
===Opened/Closed===
: 05000354/2006-005-00 LER Drywell Hoist Breaker Not Open Prior to Mode 2 Entry (Section 4OA3.2)


===Closed===
===Closed===
: [[Closes finding::05000354/FIN-2006015-03]]URIInspection of PRA Quality Issues, and NRC Reviewof HEP Assigned Value for Battery Charger Cross-
: 05000354/2006015-03 URI Inspection of PRA Quality Issues, and NRC Review of HEP Assigned Value for Battery Charger Cross-
tie Operator Action (Section 4OA5.2)  
tie Operator Action (Section 4OA5.2)
: A-2Attachment


===Discussed===
===Discussed===
None
None
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
In addition to the documents identified in the body of this report, the inspectors reviewed thefollowing documents and records:Hope Creek Generating Station (HCGS) Updated Final Safety Analysis ReportTechnical Specification Action Statement Log (SH.OP-AP.ZZ-108)
: HCGS Nuclear Controls Operator (NCO) Narrative Logs
: HCGS Plant Status Reports Weekly Reactor Engineering Guidance to Hope Creek Operations Hope Creek Operations Night Orders and Temporary Standing Orders
==Section 1R01: Adverse Weather ProtectionProceduresSH.OP-DG.ZZ-0011, Rev. 5, Station Seasonal Readiness GuideHC.OP-AB.MISC-0001, Rev. 8, Acts of Nature==
: HC.OP-GP.ZZ-0003, Rev. 18, Station Preparations for Winter Conditions
: NC.OP-DG.ZZ-0002, Rev. 6, Severe Weather GuideNotifications203138002031399120317773
: Other DocumentsDE-CB.EA/EP/EQ-0052, Rev. 2, Configuration Baseline Documentation for Station ServiceWaterHope Creek Winter/Grassing Readiness Report and Weekly Update InformationSection 1R04: Equipment AlignmentProceduresHC.OP-AB.ZZ-0172, Rev. 2, Loss of 4.16KV Bus 10A403 C ChannelHC.OP-GP.PB-0003, Rev. 11, 4.16KV Bus 10A403 Removal And Return To Service - C
: ChannelHC.OP-AP.ZZ-0108, Rev. 27, Operability Assessment and Equipment Control Program
: HC.OP-SO.EA-0001, Rev. 29, Service Water System Operation
: HC.OP-SO.EP-0001, Rev. 15, Service Water Traveling Screens System Operation
: HC.OP-SO.EG-0001, Rev. 38, Safety & Turbine Auxiliaries Cooling Water System Operation
: HC.OP-SO.GJ-0001, Rev 44, Control Area Chilled Water System OperationHC.OP-SO.GU-0001, Rev 23, Filtration, Recirculation and Ventilation System OperationHC.OP-SO.GK-0001, Rev 11, Control Area Ventilation System OperationHC.OP-ST.KJ-0003, Rev. 61, Emergency Diesel Generator 1CG400 Operability Test - Monthly
: A-3Attachment Completed SurveillancesHC.OP-ST.KJ-0002, Emergency Diesel Generator 1BG400 Operability Test - Monthly, dated2/16/07HC.OP-ST.KJ-0004, Emergency Diesel Generator 1DG400 Operability Test - Monthly, dated
: 2/19/07DrawingsM-90-1, Sheet 2, Rev 20, Auxiliary Building Control Area Chilled Water Systems, Control Area Chillers
: M-90-1, Sheet 3, Rev 17, Auxiliary Building Control Area Chilled Water System
: M-78-1, Sheet 1, Rev 15, Aux. Bldg. Control Area Air Flow DiagramNotifications201746512031409920314131203142292031444220317161203173062031400620315597203156122031589320317545
: 2031769420317939Orders301350806006820760068187501026965010269750102711
: Other DocumentsWCD 4193678
==Section 1R05: Fire ProtectionProceduresHope Creek Pre-Fire Plan==
: FRH-II-412, Rev. 3, RCIC Pump & Turbine Room, RHR Pump & HeatExchanger Rooms & Electrical Equipment Room Elevation: 54'-0" Hope Creek Pre-Fire Plan
: FRH-II-571, Rev. 5, HVAC Equipment Rooms Elevation: 178' & 199' Hope Creek Pre-Fire Plan
: FRH-II-563, Rev. 6, Control Area HVAC Equipment RoomsElevations: 155'-3" & 175'-0"Hope Creek Pre-Fire Plan
: FRH-II-552, Rev. 7, Control Room & Electrical Access Area Elevation:137'-0"Hope Creek Pre-Fire Plan
: FRH-III-133, Rev. 6, Turbine Building Elevation: 102'-0"Hope Creek Pre-Fire Plan
: FRH-II-531, Rev. 7, Diesel Generator Rooms, Elevation: 102'-0" Hope Creek Pre-Fire Plan
: FRH-II-471, Rev. 3, Refuel Floor, Elevation: 201'-0" Hope Creek Pre-Fire Plan
: FRH-II-424, Rev. 3, MCC Area, Elevation: 77'-0" Hope Creek Pre-Fire Plan
: FRH-II-431, Rev. 3, MCC Area, Elevation: 102'-0" Hope Creek Pre-Fire Plan
: FRH-II-151, Rev. 4, Turbine Building, Elevation: 137'-0"
: HC.FP-AP.ZZ-0004, Rev. 10, Actions for Inoperable Fire Protection - Hope Creek Station Salem and Hope Creek Fire Impairment Log Book, dated 2/23/07
: HC.FP-SV.ZZ-0056, Rev. 3, Fire Barrier Inspection
: HC.FP-SV.KC-0066, Rev. 3, Control Room Halon Storage Cylinders Volume Check
: HC.FP-ST.KC-0048, Halon System Air Flow Test, dated 4/14/06
: HC.FP-SV.KC-0066, Control Room Halon Storage Cylinders Volume Check, dated 5/21/06 &11/15/06
: A-4Attachment Notifications203138842031393920314142203144042031454320314545202463332031398520314098203143952031443420314544
: 246331202463342024633520319478Other DocumentsWCD 4196769
==Section 1R06: Flood Protection MeasuresProceduresHC.RW-FT.HB-0001, Rev. 0, Sump Pump Status Check - MonthlyHC.RW-SO.HG-0001, Rev. 5, Radioactive Drains and Waste System Operation==
: HC.ER-DG.ZZ-0002, Rev. 2, System Function Level Maintenance Rule Scoping vs. RiskReferenceCalculationsCALC. No. 11-92, Rev. 5, Reactor BLDG Flooding -
: EL 54' & 77'CALC. No. 11-0067, Rev. 1, High Energy Line Break Analysis in Reactor BuildingCompleted SurveillancesHC.OP-IS.SK-0101, dated 3/9/07, Plant Leak Detection System Valves - Inservice Test DrawingsM-97-1
: SH.2, Rev. 15, Building and Equipment Drain Reactor Building Notifications201844692018880320198042202168832023626620263789202814732028415820287943203002102030996620313916Orders70047610700476517005219370062469301087443011970430146717600455256005079460067964Other DocumentsCALC. No. 11-92, Rev. 5, Reactor BLDG Flooding -
: EL 54' & 77'CALC. No. 11-0067, Rev. 1, High Energy Line Break Analysis in Reactor Building Completed Surveillance
: HC.OP-IS.SK-0101, dated 3/9/07, Plant Leak Detection System Valves
- Inservice Test Hope Creek Generating Station Individual Plant Examination, dated April 1994Operating ExperienceNRC Information Notice 92-69: Water Leakage from Yard Area Through Conduits into Buildings,dated 9/22/92NRC Information Notice 98-31: Fire Protection System Design Deficiencies and Common-ModeFlooding of Emergency Core Cooling System Rooms at Washington Nuclear Project Unit
: 2, dated 8/18/98 
: A-5Attachment NRC Information Notice 2005-11: Internal Flooding/Spray-Down of safety-Related EquipmentDue to unsealed Equipment hatch Floor Plugs and/or Blocked Floor Drains, dated 5/6/05
==Section 1R11: Licensed Operator Requalification ProgramProceduresSH.OP-AS.ZZ-0001, Rev. 13, Operations StandardsHC.OP-AP.ZZ-0108, Rev. 27, Operability Assessment and Equipment Control Program==
: HC.OP-AB.ZZ-0000, Rev. 3, Reactor Scram
: HC.OP-AB.COOL-0001, Rev. 11, Station Service Water
: HC.OP-AB.COOL-0002, Rev. 1, SACS / TACS Cooling
: HC.OP-AB.BOP-0002, Rev. 7, Main Turbine
: HC.OP-EO.ZZ-0101FC, Rev. 10, Reactor Pressure Vessel (RPV) Control Flow Chart
: HC.OP-EO.ZZ-0102FC, Rev. 11, Primary Containment Control Flow ChartNotifications203139152031424920314006
: Other DocumentsHCGS Event Classification Guide and ProceduresCompleted Emergency Classification Paperwork
==Section 1R12: Maintenance EffectivenessProceduresHC.ER-DG.ZZ-0002, Rev. 2, System Function Level Maintenance Rule Scoping Vs. RiskReference==
: HC.OP-ST.GS-0003, Rev. 5, Reactor Building/Suppression Chamber Vacuum Breaker Operability Test - MonthlyDrawingsM-57-1, Rev. 25, Containment Atmosphere Control Notifications203078852031391620314363203163522031653220317017203175292031753020317546203176652031772320317954
: 20318002203180032030923620308540Orders7006494870064928
: Other DocumentsContainment Atmosphere Control Maintenance Rule Availability Graphs (October 2005 - January
: 2007)
: IST Component Requirement for 1-GS-HV-5029
: IST Component Requirement for 1-BC-HV-F007A
: A-6Attachment
==Section 1R13: Maintenance Risk Assessments and Emergent Work ControlProceduresHC.OP-AP.ZZ-0108, Rev. 27, Operability And Equipment Control ProgramSH.OP-AP.ZZ-0027, Rev. 12, On-Line Risk Assessment==
: HC.ER-DG.ZZ-0002, Rev. 2, System Function Level Maintenance Rule Scoping vs. Risk Reference
: HC.OP-AB.ZZ-0172, Rev. 2, Loss of 4.16KV Bus 10A403 C Channel
: HC.OP-GP.PB-0003, Rev. 11, 4.16KV Bus 10A403 Removal And Return To Service - C
: Channel
: HC.OP-ST.KJ-0003, Rev. 61, Emergency Diesel Generator 1CG400 Operability Test - Monthly
: HC.OP-AB.COMP-0001, Rev. 2, Instrument and/or Service Air
: HC.OP-AB.COMP-0002, Rev. 4, Primary Containment Instrument Gas
: HC.OP-AB.BOP-0006, Rev. 9, Main Condenser Vacuum
: HC.OP-AB.BOP-0003, Rev. 3, Turbine Hydraulic Pressure
: HC.OP-SO.CH-0001, Rev. 37, Main Turbine Control Oil (EHC) System OperationCompleted SurveillancesHC.OP-ST.ZZ-0001, dated 3/9-12/07, Power Distribution Lineup- Weekly Notifications2031559720315612203158932031372220313763203144192031795620318063203158912031803120318936Orders501020675010206830101292301350806006820760068187501026965010269750102711301467173014901060068538Other DocumentsHCGS PRA Risk Evaluation Forms for Work Week Nos. 701 - 713HCGS Relay Test Orders
: HCGS Relay Work Standards
: WCDs
: 4192439,
: 4192977, 4193678
: Completed Surveillance
: HC.OP-ST.ZZ-0001, dated 3/9-12/07, Power Distribution Lineup-
: Weekly
==Section 1R15: Operability EvaluationsProceduresHC.OP-SO.AF-0001, Rev. 33, Extraction Steam, Heater Vents and Drains System OperationHC.OP-DL.ZZ-0005, Rev. 39, Attachment 9, Operator Action for==
: FWH Level Outside Normal BandHC.OP-ST-BB-0001, Rev. 35, Recirculation Jet Pump Operability - Daily
: HC.OP-AP.ZZ-0108, Rev. 27, Operability Assessment and Equipment Control Program
: HC.OP-AB.IC-0001, Rev. 6, Control Rod
: A-7Attachment Completed SurveillancesHC.OP-ST.BF-0002, dated 3/27/07, Control Rod Drive Accumulator Operability Check - WeeklyDrawingsM-04-1, Rev.11, Vents & Drains Heaters 3,4,5 & 6E-0018-1, Sh. 1, Rev. 21, Single Line Meter & Relay Diagram 480 Volt Class 1E Unit Substation
: 10B410, 10B420, 10B430, 10B440, 10B450, 10B460, 10B470, 10B480
: M-11-1, Sh. 1, Rev. 29, Safety Auxiliaries Cooling Reactor Building
: 1-P-EG-06, Sh. 1, Rev. 15, System Isometrics / Reactor Bldg. Safety Auxiliary Cooling System
'A' Pump and Heat Exchangers
: FSK-P-1-EA-664-22, Sh. 2, Rev. 22, Small Piping/Intake Structure Lubrication Line From 10T-
: 544 to Valves
: SV-2247B & SV-247D
: M-10-1, Sh. 3, Rev. 27, Service WaterNotifications203088142030883920308817203132432031311720293016202982532031080020307589202981602028786020292989
: 203153642031530620308114203080412031422320314302
: 2031437820314455203144592031379120314104Orders700418987006498370066093600674907006626130118865700601587005868360068125500892397006455160066868
: 60067964700665807006661480091785Other DocumentsVTD 10855-M-010, Instructions for Installation, Operation, and Maintenance of ClosedFeedwater HeatersHCGS UFSAR Section 6.8, Filtration, Recirculation, and Ventilating Systems
: HCGS UFSAR Section 9.4, Air Conditioning, Heating, Cooling, and Ventilating Systems
: VTD
: PN1-A41-8010-0042, Rev. 6,
: GEK-90333A, Reactor Recirculation System Operating andMaintenance Instructions50.59 Review Form for Rev. 35 to HC.OP-ST-BB-0001
'B' FRVS Charcoal Radioiodine Test Report Dated March 8, 2007DEH070001, Technical Evaluation for Pipe Hanger Restraint Pin Missing in Hope Creek1-P-EA-142-C001, Design Calculation for Service Water, Lube Water Supply Header andSupports 1-P-EA-142-H01 & H02NRC Inspection Manual Chapter 9900 Technical Guidance: Operability Determinations &
: F
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: A-8Attachment
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: A
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: R
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: A-10Attachment
/2
/
: 5NRC Generic Letter 90-05: Guidance For Performing Temporary Non-Code repair of ASMECode Class 1, 2,, and 3 Piping, dated 6/15/90Condition Resolution Operability Determination Notebook
: SH.MD-GP.ZZ-0240, System pressure Test Data Sheet, dated 2/23/07Section 1R17: Permanent Plant ModificationsProceduresHC.OP-SO.DA-0001, Rev. 37, Circulating Water System OperationDrawingsE-0203-0, Rev. 3, Cooling Tower Basin Miscellaneous Valve & Intake Structure Deicing ValveJ-09-0, sheet 19, Rev. 2, Circulating Water System Intake Structure Deicing ValvesOrders6006556180090515
: Other DocumentsCalculation
: EA-0020, Deicing Line Hydraulics
==Section 1R19: Post-Maintenance TestingProceduresER-AA-430, Rev. 2, Conduct of Flow Accelerated Corrosion ActivitiesER-HC-430-9055, Rev. 0, Hope Creek Conduct of Flow Accelerated Corrosion Activities==
: ER-AA-430-1001, Rev. 2, Guidelines for Flow Accelerated Corrosion Activities
: HC.MD-CM.BB-0008, Rev. 1, Reactor Recirculation Pump N-7500 Mechanical Seal Rebuild
: HC.MD-CM.BB-0003, Rev. 17, Reactor Recirculation Pump Seal Changeout
: NC.NA-AP.ZZ-0050, Rev. 7, Station Post Maintenance Testing
: NC.MD-AP.ZZ-0050, Rev. 9, Maintenance Testing Program Matrix
: SH.MD-AP.ZZ-0003, Rev. 17, Maintenance Department Written Instruction Use Standard
: HC.IC-GP.ZZ-0031, Rev. 16, Bailey / NLI Logic Module, Type 862
: HC.IC-GP.ZZ-0070, Rev. 5, Bailey Fuse Module, Type 862
: SH.MD-EU.ZZ-0002, Rev. 1, Coupling Alignment
: SH.MD-GP.ZZ-0240, Rev. 7, System Pressure Test at Normal Operating Pressure and TemperatureDrawings
: A-11Attachment M-02-1, Rev.13, Extraction SteamM-43-1, Sh. 1, Rev. 31, Reactor Recirculation
: M-10-1, Sh. 2, Rev. 36, Service Water
: M-15-0, Sh. 5, Rev. 6, Compressed Air (Instrument)Notifications202838862031140620311515203136542030826720307673202857452025129020281533203091612029947720240048
: 203160082031375020313869203139222031424720314417
: 20317835Orders700574056006686660063938301396148009155160066957700501176005712970050000700500186006694070056604
: 500820465008204250082043600669556006717060056618
: 800834986006577960055819Other DocumentsClearance Order 4021446MPR Associates 3A Feedwater Heater Pipe Tee Temporary Repair Analysis, Dated January 27, 2007Ultrasonic Test Results for 3A and 3C Feedwater Heater Pipe Tees Design Change Package
: 80083498, Replacement of SSW Emergency Isolation Drain Valves with AOVs
: VTD PM0150Q-0050, Rev. 2, Primary Containment Vacuum Relief Valve Instruction Manual
: VTD PJ200Q-2385, Rev. 12, 862 - Cabinet Layout BC652-9
: VTD PJ200Q-0384, Rev. 6, 862 System Containment Atmosphere Control H2/O2 Analyzer IslnValve
: HV-4955BVTD PJ200Q-0392, Rev. 6, 862 System Containment Atmosphere Control H2/O2 Analyzer IslnValve
: HV-5019BVTD PJ200Q-0389, Rev. 7, 862 System Containment Atmosphere Control H2/O2 Analyzer IslnValve
: HV-4959BVTD PJ200Q-0393, Rev. 8, 862 System Containment Atmosphere Control H2/O2 Analyzer IslnValve
: HV-4966BVTD PJ200Q-1479, Rev. 6, 862 System Containment Atmosphere Control H2/O2 Analyzer IslnValve Intlk. Ch. 6
==Section 1R20: Refueling and Outage ActivitiesProceduresHC.OP-SO.AE-0001, Rev. 45, Feedwater System OperationHC.OP-IO.ZZ-0002, Rev. 46, Preparation for Plant Startup==
: HC.OP-IO.ZZ-0003, Rev. 75, Startup from Cold Shutdown to Rated Power
: HC.OP-IO.ZZ-0004, Rev. 68, Shutdown from Rated Power to Cold Shutdown
: HC.OP-IO.ZZ-0007, Rev. 22, Operations from Hot Standby
: HC.OP-IO.ZZ-0010, Rev. 6, Scram Recovery
: HU-AA-101, Rev. 3, Human Performance Tools and Verification Practices
: 2Attachment DrawingsM-05-1, Sh. 2, Rev. 23, CondensateNotifications2031149420311443203115532031174320311390203114222031153620311425203136562028574520308267Orders6006743580091551600669576006686670065696
: Other DocumentsShutdown Safety Assessment Report for Planned Outage (F71) scheduled to begin 01/26/07and end 1/30/07
: Planned Outage Shutdown and Startup Fuel Defect Sampling Plan
: 10855-D3.28, Design, Installation and Test Specification of the Nuclear Boiler System Ultrasonic Thickness Examination Records D-58M / D-54B and D-1M / D-1B
==Section 1R22: Surveillance TestingProceduresHC.OP-IS.BJ-0001, Rev. 48,==
: HPCI Main and Booster Pump Set - 0P204 and 0P217 - InserviceTest
: HC.OP-ST.KJ-0002, Rev. 61, Emergency Diesel Generator 1BG400 Operability Test - Monthly
: HC.OP-ST.KJ-0015, Rev. 24, EDG 1BG400 - 24 Hour Operability Run and Hot Restart Test
: HC.OP-ST.BE-0002, Rev. 40, B & D Core Spray Pumps - BP206 and DP206 - In-Service Test
: HC.OP-ST.BF-0001, Rev. 23, Control Rod Scram Time Surveillance
: HC.MD-ST.PK-0002, Rev 29, 125 Volt Quarterly Battery SurveillanceDrawingsM-55-1, Sh. 1, Rev. 38, High Pressure Coolant InjectionM-56-1, Sh. 1, Rev. 31, HPCI Pump Turbine
: E-0009-1, Single Line Meter & Relay Diagram, 125V DC System Channels C & DNotifications203103732030991820296659202862402031372820314020203142522031430520290840202924882029567220299811
: 203086262029973020292871202924322031608020316111
: 2031640420293974Orders500997365010147050087561501016746006499550099699
: 70055909Other DocumentsH-1-BE-NEE-0506, Seismic Evaluation of the Vibration Damper and Absorber Installed on theCore Spray Pumps, 1BP206 and 1DP206
: H-1-BE-SDC-0739, Core Spray Pump Absorber Decoupling Evaluation
: A-13Attachment
==Section 1R23: Temporary Plant ModificationsProceduresNC.CA-DG.ZZ-0103, Rev. 1, Adverse Condition Monitoring and Contingency PlanningDrawingsE-0436-0, Sh. 1, Rev. 7, Electrical Schematic Diagram 4.16KV Class 1E Ckt. Brkr. ControlChiller Compressor Motor 1AK400==
: E-0436-0, Sh. 2, Rev. 8, Electrical Schematic Diagram 4.16KV Class 1E Ckt. Brkr. Control Chiller Compressor Motor 1AK400Notifications
: 20315548
: Orders8009194660068169
: Other DocumentsVTD PM723Q-0013, Sh. 1, Rev. 13, 19FA Electronic Control Diagram for Nuclear Plant DutyVTD PM723Q-0017, Sh. 0, Rev. 5, Logic Control Annunciation Diagram for 19FQ Machine EmergencySection 1EP2: Alert and Notification System TestingOther DocumentsFinal Rep - 10 Design Review ReportSiren Test Results from 2006 & 2007 (bi-weekly silent test & quarterly audible test)
: Maintenance Records from November 2005
==Section 1EP3: Emergency Response Organization AugmentationOther DocumentsSalem/Hope Creek Emergency PlanERO Member RosterSection 1EP4: Emergency Action Level and Emergency Plan ChangesOther DocumentsAll 50.54(q)==
: E-Plan and EAL changes from 2005 & 2006
==Section 1EP5: Correction of Emergency Preparedness Weaknesses and DeficienciesOrders7005330870053597700539737005404770054318Other Documents==
: A-14Attachment
: LS-AA-120 "Issue Identification and Screening Process," Rev. 6LS-AA-125 "Corrective Action Program (CAP) Procedure," Rev. 11
: All Issue Reports related to EP from 12/19/05 - 3/27/07
: Drill Critique Reports - 2005 & 2006
: 50.54(t) Audits done by the Nuclear Oversight Committee (2006 & 2007)
==Section 1EP6: Drill EvaluationProceduresSH.OP-AS.ZZ-0001, Rev. 13, Operations StandardsHC.OP-AP.ZZ-0108, Rev. 27, Operability Assessment and Equipment Control Program==
: HC.OP-AB.ZZ-0000, Rev. 3, Reactor Scram
: HC.OP-AB.COOL-0001, Rev. 11, Station Service Water
: HC.OP-AB.COOL-0002, Rev. 1, SACS / TACS Cooling
: HC.OP-AB.BOP-0002, Rev. 7, Main Turbine
: HC.OP-EO.ZZ-0101FC, Rev. 10, Reactor Pressure Vessel (RPV) Control Flow Chart
: HC.OP-EO.ZZ-0102FC, Rev. 11, Primary Containment Control Flow ChartNotifications
: 20314006
: Other DocumentsHCGS Event Classification Guide and ProceduresCompleted Emergency Classification Paperwork
==Section 2OS1: Access Control to Radiologically Significant AreasProceduresRP-AA-460, Rev. 11, Controls for High and Very High Radiation AreasRP-AA-460,-1001 Rev. 1, Additional High Radiation Exposure ControlsNotifications2030743220306791Section 2OS2:==
: ALARA Planning and ControlsProceduresRP-AA-270, Rev 3, Prenatal Radiation ExposureRP-AA-220, Rev 3, Bioassay Program
: RP-AA-222, Rev 1, Methods for estimating Internal Exposure from In Vivo and In Vitro Bioassay DataRP-AA-400, Rev 4, ALARA Program
: RP-AA-401, Rev 7, Operational ALARA Planning and ControlsOther DocumentsALARA Review 2007-25, "A" Rx Recirc Pump Activities
: A-15Attachment Micro ALARA Review 2007-27, Drywell EPU Strain Guage RepairSection 2OS3: Radiaiton Monitoring InstrumentationProceduresRP-AA-1001, Rev 0, Establishing Collective radiation Exposure Estimates and Goals
==Section 4OA1: Performance Indicator VerificationProceduresLS-AA-2001, Rev. 4, Collecting and Reporting of==
: NRC Performance Indicator DataLS-AA-2010, Rev. 4, Monthly Data Elements for NRC/WANO Unit/Reactor Shutdown Occurrences
: LS-AA-2030, Rev. 4, Monthly Data Elements for NRC Unplanned Power Changes per 7000
: Critical Hours
: EP-AD-022, " Nuclear Emergency Planning Performance Indicators," Rev. 2Other DocumentsMonthly Operating Reports for the Months of February 2005 through January 2007Hope Creek NRC Performance Indicators, First Quarter 2005 through Fourth Quarter 2006
: ERO Drill Participation PI data, 1Q06, 2Q06, 3Q06 & 4Q06
: Public Notification System PI data, 1Q06, 2Q06, 3Q06 & 4Q06
: DEP PI data, 1Q06, 2Q06, 3Q06 & 4Q06Section 4OA2: Identification and Resolution of ProblemsProceduresHC.IC-AP.ZZ-00017, Rev. 0, Bailey Module Reliability ProgramHC.SE-PR.RL-0001, Rev. 6, Bailey 862 Logic Module Trending ProgramNotifications202992212028215420299528203139692027316520273515202798402027984320279959 202631912024634520239521
: 2665902026206320308741203085402026702420251290Orders600668606005953960061981600657796006578060065457600611837005456570062185700664638008939880080950
: 800786548008058370052075700493087004802170052848
: 8008689070064948600668597005000070050018Other DocumentsRL System Engineer Bailey Solid State Logic Module Failure TrendingVTD PJ200Q-0599, Sh. 0, Rev. 13, 4.16KV System Diesel Generator Circuit Breaker (1)52-
: 40407
: PSEG Electronic System Health Indicator Program (eSHIP)
: A-16Attachment
==Section 4OA3: Event FollowupProceduresHC.OP-SO.AE-0001, Rev. 45, Feedwater System OperationHC.OP-IO.ZZ-0002, Rev. 46, Preparation for Plant Startup==
: HC.OP-IO.ZZ-0003, Rev. 75, Startup from Cold Shutdown to Rated Power
: HC.OP-IO.ZZ-0004, Rev. 68, Shutdown from Rated Power to Cold Shutdown
: HC.OP-IO.ZZ-0007, Rev. 22, Operations from Hot Standby
: HC.OP-IO.ZZ-0010, Rev. 6, Scram Recovery
: HU-AA-101, Rev. 3, Human Performance Tools and Verification PracticesDrawingsM-05-1, Sh. 1, Rev. 24, CondensateM-05-1, Sh. 2, Rev. 23, Condensate
: M-06-1, Sh. 1, Rev. 25, Feedwater
: M-16-1, Sh. 1, Rev. 31, Condensate Demineralizer
: M-41-1, Sh. 1, Rev. 35, Nuclear BoilerNotifications203136562028574520308267
: Orders80091551600669576006686670065696
: Other Documents10855-D3.28, Design, Installation and Test Specification of the Nuclear Boiler SystemUltrasonic Thickness Examination Records D-58M / D-54B and D-1M / D-1B
: Low Reactor Water Level Scram Root Cause Evaluation Plant Computer System Data Trends


==Section 4OA5: Other ActivitiesProceduresNC.MD-PM.DCS-0003, Rev. 3, Sealing, Drying, and Backfilling of a Loaded==
: MPCNotifications2030716420304882
: Orders6006392970063881
: Other DocumentsDCS Hose Failure During Blowdown and associated Prompt Investigation ReportContamination Found on
: HI-TRAC and associated Apparent Cause Report Dry Cask Storage Lessons Learned Action Items, Canister #1, dated 11/6/2006
: Dry Cask Storage Post Job Critique Action Item List, dated 2/7/2007
: A-17Attachment ALARA Post Job Reviews, Dry Cask Storage Activities, Casks 1-4Dry Cask Storage Notification SummarySection 4OA7: Licensee-Identified ViolationsProceduresHC.OP-IO.ZZ-0002, Rev 47, Preparation for Plant StartupNotifications
: 20307894
: Orders 70064553
: Other DocumentsRoot Cause Investigation Report, 10-H-202 Drywell Hoist Breaker Not Open Prior to Mode 2 Entry
: HCGS Licensee Event Report 2006-005-00, Dated February 16, 2007
: A-18Attachment
==LIST OF ACRONYMS==
ADAMSAgencywide Documents Access and Management SystemALARAAs Low As Is Reasonably Achievable
ANSAlert and Notification System
ANSI/ANSAmerican National Standards Institute / American Nuclear Society
CAPCorrective Action Program
CEDECommitted Effective Dose Equivalent
CFRCode of Federal Regulations
CRControl Room
DCSDry Cask Storage
DEPDrill and Exercise Performance
EALEmergency Action Level
ECCSEmergency Core Cooling Systems
EDGEmergency Diesel Generator
EHCElectro-Hydraulic Control
: [[EOFE]] [[mergency Operations Facility]]
: [[EP]] [[Emergency Preparedness]]
EROEmergency Response Organization
FRVSFiltration, Recirculation, and Ventilation System
HCGSHope Creek Generating Station
HEPHuman Error Probability
HPCIHigh Pressure Coolant Injection
HVACHeating, Ventilation and Air Conditioning
IMCInspection Manual Chapter
ISFSIIndependent Spent Fuel Storage Installation
LERLicensee Event Report
LOOPLoss of Offsite Power
MCCMotor Control Center
MPCMulti Purpose Canister
MRMaintenance Rule
MSPIMitigating System Performance Index
NCONuclear Controls Operator
NCVNon-cited Violation
NEINuclear Energy Institute
NRCNuclear Regulatory Commission
OAOther Activities
PARSPublicly Available Records
PIsPerformance Indicators
PRAProbabilistic Risk Assessment
: [[PSEGP]] [[ublic Service Enterprise Group Nuclear]]
: [[LLC]] [[]]
RACSReactor Auxiliaries Cooling System
RCICReactor Core Isolation Cooling
RHRResidual Heat Removal
RPVReactor Pressure Vessel
SACSSafety Auxiliaries Cooling System
SRASenior Reactor Analyst
A-19Attachment SRVSafety Relief ValveSSCsStructures, Systems, and Components
SSWStation Service Water
TACSTurbine Auxiliaries Cooling System
UFSARUpdated Final Safety Analysis Report
URIUnresolved Item
VHRAVery High Radiation Areas
: [[WCDW]] [[ork Clearance Document]]
}}
}}

Latest revision as of 23:47, 14 January 2025

IR 05000354-07-002, on 01/01/2007 - 03/31/2007; Hope Creek Generating Station; Resident Inspector Integrated Report
ML071290407
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 05/09/2007
From: Arthur Burritt
Reactor Projects Branch 3
To: Levis W
Public Service Enterprise Group
BURRITT, AL
References
IR-07-002
Download: ML071290407 (43)


Text

May 9, 2007

SUBJECT:

HOPE CREEK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000354/2007002

Dear Mr. Levis:

On March 31, 2007, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Hope Creek Generating Station. The enclosed integrated inspection report documents the inspection results, which were discussed on April 5, 2007, with Mr. George Barnes and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no findings of significance were identified. However, licensee-identified violations which were determined to be of very low safety significance are listed in this report. The NRC is treating these violations as non-cited violations (NCVs)

consistent with Section VI.A.1 of the NRC Enforcement Policy because of the very low safety significance of the violations and because they are entered into your corrective action program.

If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Hope Creek Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the

Mr. NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Arthur L. Burritt, Chief Projects Branch 3 Division of Reactor Projects Docket No:

50-354 License No:

NPF-57 Enclosure:

Inspection Report 05000354/2007002 w/Attachment: Supplemental Information cc w/encl:

G. Barnes, Site Vice President D. Winchester, Vice President - Nuclear Assessments B. Clark, Director - Finance J. Perry, Hope Creek Plant Manager J. J. Keenan, General Solicitor, PSEG M. Wetterhahn, Esquire, Winston and Strawn, LLP Consumer Advocate, Office of Consumer Advocate, Commonwealth of Pennsylvania L. A. Peterson, Chief of Police and Emergency Management Coordinator P. Baldauf, Assistant Director of Radiation Protection Programs, State of New Jersey K. Tosch, Chief, Bureau of Nuclear Engineering, NJ Dept. of Environmental Protection H. Otto, Ph.D., Administrator, Interagency Programs, DNREC Division of Water Resources, State of Delaware N. Cohen, Coordinator - Unplug Salem Campaign E. Zobian, Coordinator - Jersey Shore Anti Nuclear Alliance

M

SUMMARY OF FINDINGS

IR 05000354/2007002; 01/01/2007 - 03/31/2007; Hope Creek Generating Station; Resident

Inspector Integrated Report.

The report covered a 13-week period of inspection by resident inspectors, regional health physicist inspectors, and regional reactor inspectors. No findings of significance were identified.

The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

NRC-Identified and Self-Revealing Findings

No findings of significance were identified.

Licensee Identified Violations

Violations of very low safety significance, that were identified by Public Service Enterprise Group (PSEG) have been reviewed by the inspectors. Corrective actions taken or planned by PSEG have been entered into PSEG's corrective action program. These violations and corrective actions are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

The Hope Creek Generating Station began the first quarter operating at 100% power. The plant was shutdown on January 26, 2007, to cold shutdown conditions to execute a scheduled maintenance outage.

During power ascension on January 29, 2007, Hope Creek automatically scrammed on low reactor water level caused by a failed reactor feed pump minimum flow valve. The plant was returned to 100% power on February 2, 2007, and remained at or near full power for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a.

Inspection Scope (1 sample)

The inspectors reviewed seasonal adverse weather preparation activities related to river grass intrusion conditions that impact the station service water system. Inspectors assessed implementation of PSEGs grassing readiness plan through plant walkdowns, corrective action program review, and discussions with cognizant managers and engineers. Documents reviewed by inspectors are listed in the attachment.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdown (5 samples)

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems to verify the operability of redundant or diverse trains and components when safety equipment was inoperable. The inspectors completed walkdowns to identify any discrepancies that could impact the function of the system, and therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control systems components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that PSEG had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program. Documents reviewed are listed in the attachment.

C A and C 1E switchgear during planned maintenance on the B 1E switchgear C

Redundant station service water (SSW) trains and support equipment during maintenance on the D SSW pump and traveling water screen C

The A & C SSW trains, emergency diesel generators (EDGs), and 4KV switchgear rooms during the emergent unavailability of the B & D SSW trains C

Redundant EDG, emergency core cooling systems (ECCS), SSW, filtration, recirculation, and ventilation system (FRVS), station auxiliary cooling system (SACS), and control room (CR) chilled water equipment during extended planned maintenance on the C EDG and unplanned unavailability of the B FRVS vent fan and A CR chiller C

B control room chilled water system after return to service following extended planned maintenance

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Fire Protection - Quarterly Tours

a.

Inspection Scope (10 samples)

The inspectors conducted tours of ten areas to assess the material condition and operational status of fire protection features. The inspectors verified that combustible material and ignition sources were controlled in accordance with PSEGs administrative procedures; fire detection and suppression equipment was available for use; that passive fire barriers were maintained in good material condition; and that compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with PSEGs fire plan. The areas toured are listed below with their associated pre-fire plan designator. Other documents reviewed are listed in the attachment.

C FRH-II-571, diesel area heating, ventilation and air conditioning (HVAC)equipment room C

FRH-II-563, control area HVAC equipment rooms C

FRH-II-552, control room area C

FRH-III-133, accessible turbine building rooms containing offsite power source bus ducts to safety-related 4KV busses C

FRH-II-412, D residual heat removal (RHR) pump and reactor core isolation cooling (RCIC) pump rooms C

FRH-II-531, Common EDG Corridor, 102' Elevation C

FRH-II-471, Refuel Floor, 201' Elevation C

FRH-II-424, Motor Control Center (MCC) Area, Room 4218, 77' Elevation C

FRH-II-431, MCC Area, Room 4303, 102' Elevation C

FRH-II-151, A Recirc MG Set Room, 137' Elevation

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

.1 Internal Flooding

a.

Inspection Scope (1 sample)

The inspectors reviewed selected risk-important plant design features and PSEG procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors focused on mitigation strategies and equipment in the B RHR pump room. The inspectors reviewed flood analysis and design documents, including the updated final safety analysis report, engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis. In addition, the inspectors walked down the B RHR room and adjacent rooms in the reactor building to assess potential flooding vulnerabilities.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Requalification Activities Review By Resident Staff

a.

Inspection Scope (1 sample)

The resident inspectors observed one annual licensed operator requalification simulator examination scenario on January 20, 2007, to assess operator performance and training effectiveness. The scenario involved a main turbine vibration problem, a failed reactor mode switch, and a steam leak in the turbine building. The inspectors assessed simulator fidelity and observed the simulator instructors critique of operator performance.

The inspectors also observed control room activities with emphasis on simulator identified areas for improvement. Finally, the inspectors reviewed applicable documents associated with licensed operator requalification as listed in the attachment.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a.

Inspection Scope (3 samples)

The inspectors reviewed the three samples listed below for items such as:

(1) appropriate work practices;
(2) identifying and addressing common cause failures; (3)scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR);
(4) characterizing reliability issues for performance;
(5) trending key parameters for condition monitoring;
(6) charging unavailability for performance;
(7) classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2); and
(8) appropriateness of performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Documents reviewed are listed in the attachment. Items reviewed included the following:

C A RHR pump minimum flow valve failed to close; C

GS-HV-5029 reactor building to suppression chamber vacuum breaker isolation valve slow closure; and C

C reactor auxiliaries cooling system (RACS) pump motor failure.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope (5 samples)

The inspectors reviewed on-line risk management evaluations through direct observation and document reviews for the following configurations:

C Planned maintenance on the A EDG on January 3, 2007; C

B 1E switchgear relay outage testing reclassified as online and performed on February 8, 2007; C

Concurrent planned maintenance on the D SSW pump, A circulating water pump, B primary containment instrument gas compressor, and the 10K107 service air compressor on February 20-22, 2007; C

Unplanned unavailability of the B FRVS vent fan and A control room chiller during planned extended maintenance on the C EDG on March 7, 2007; and C

Emergent unavailability of the B electro-hydraulic control (EHC) pump on March 27 and 28, 2007.

The inspectors reviewed the applicable risk evaluations, work schedules and control room logs for these configurations to verify that concurrent planned and emergent maintenance and test activities did not adversely affect the plant risk already incurred with these configurations. PSEGs risk management actions were reviewed during shift turnover meetings, control room tours, and plant walkdowns. The inspectors also used PSEGs on-line risk monitor (Equipment Out-Of-Service workstation) to gain insights into the risk associated with these plant configurations. Finally, the inspectors reviewed notifications documenting problems associated with risk assessments and emergent work evaluations. Documents reviewed are listed in the attachment.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a.

Inspection Scope (5 samples)

The inspectors reviewed five operability determinations for degraded or non-conforming conditions associated with:

C SACS pipe support failure on December 20, 2006; C

Operation of the 6B feedwater heater with water level low-out-of-specification C

on December 31, 2006; C

A control room chiller temperature control valve inoperability on February 10, 2007; C

B SSW lube water supply system through-wall leakage on February 22 - 28, 2007; and C

B FRVS vent fan unplanned inoperability on March 5, 2007.

The inspectors reviewed the technical adequacy of the operability determinations to ensure the conclusions were justified. The inspectors also walked down accessible equipment to corroborate the adequacy of PSEGs operability determinations.

Additionally, the inspectors reviewed other PSEG identified safety-related equipment deficiencies during this report period and assessed the adequacy of their operability screenings. Notifications and documents reviewed are listed in the attachment.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a.

Inspection Scope (1 sample)

The inspectors reviewed a design change associated with a valve (DA-HV-2097) in the service water structure deicing line. The modification changed the controls of the motor operator on the valve such that the valve will be not open beyond 12% of full-open. The modification was installed to limit the amount of circulating water diverted from the cooling tower basin to the service water intake structure to minimize the chance of silt disturbance near the service water pump suctions.

The design bases, licensing bases, modification instructions and post modification testing of the affected components were reviewed to verify the performance capability of this equipment was not adversely affected. The inspectors reviewed the applicable technical specifications for this equipment to ensure that operability requirements and allowable outage time limits were met. The inspectors also reviewed notifications documenting deficiencies identified related to permanent plant modifications. The documents reviewed as part of these inspections are listed in the attachment.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a.

Inspection Scope (6 samples)

The inspectors reviewed the post-maintenance tests listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed test procedures to verify the procedure adequately tested the safety functions that may have been affected by the maintenance activity and the acceptance criteria in the procedure were consistent with the Updated Final Safety Analysis Report (UFSAR) and other design or license basis documentation. The inspectors also witnessed the test or reviewed the test data to verify test results adequately demonstrated restoration of the affected safety functions. Documents reviewed are listed in the attachment.

C WO 60056618, A emergency service water makeup valve design change

  • WO 60065779, B H2/O2 analyzer isolation valves bailey card replacement
  • WO 60067170 and 60066955, repair of A and C drywell to suppression chamber vacuum breaker indications
  • WO 60055819, C EDG keepwarm pump replacement Ultrasonic measurement data associated with the 3A feedwater heater extraction steam piping was reviewed by a NRC regional specialist. The repair methods and post-maintenance testing methodology was also reviewed by the regional specialist and determined to be adequate.

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

.1 Scheduled Maintenance Outage on January 26, 2007

a.

Inspection Scope (1 sample)

The plant was shutdown on January 26, 2007, to implement a planned maintenance outage. The primary purpose of the outage was to repair a steam leak on an extraction steam line providing steam to the 3A feedwater heater and to replace the shaft seal package on the A reactor recirculation pump. The inspectors reviewed these maintenance activities and they are documented in section 1R19, Post-Maintenance Testing.

The inspectors reviewed PSEGs outage schedule and activities to verify that risk was considered appropriately and that license and technical specification requirements were adhered to. The inspectors observed portions of the reactor shutdown and subsequent start up from the control room to verify PSEG adhered to station procedures and to evaluate operator performance. The inspectors toured areas of the plant that were normally inaccessible during power operations to verify that safety related and risk significant SSCs were maintained in an operable condition. The inspectors performed a walkdown of the drywell following completion of all maintenance activities to verify there was no evidence of system leakage and that debris had not been left behind that could affect performance of plant equipment. Documents reviewed are listed in the attachment.

Hope Creek completed the scheduled maintenance outage on January 29, 2007, at 10:51 pm when the main generator was synchronized to the 500 kV grid. At 11:10 pm the reactor protection system automatically inserted all control rods into the reactor core due to a reactor pressure vessel (RPV) water level control problem. The transient is described in more detail in section 4OA3, Event Followup.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a.

Inspection Scope (5 samples)

The inspectors witnessed five surveillance tests and reviewed test data of selected surveillance tests listed below to verify that the test met the requirements of the Technical Specifications, UFSAR, and station procedures. The inspectors also determined whether the testing effectively demonstrated that the structures, systems, and components were operationally ready and capable of performing their intended safety functions. Documents reviewed are listed in the attachment.

  • WO 50101674, Class 1E, Channel D, 125 Volt Quarterly Battery Surveillance on March 21, 2007

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a.

Inspection Scope (1 sample)

The inspectors reviewed a temporary plant modification (T-Mod 07-007) associated with the A control room chiller. The modification bypassed a thrust bearing high oil temperature switch that had failed and resulted in an unplanned trip of the chiller. The inspectors verified the modification was consistent with the design and licensing bases of the chilled water system and that the performance capability of the system was not degraded by the modification. The inspectors reviewed documents to verify PSEG followed their processes for implementing temporary modifications on plant SSCs. In addition, the inspectors verified the modified equipment alignment through control room instrumentation and plant walkdowns of accessible portions of the affected equipment.

The inspectors also reviewed notifications documenting problems associated with equipment affected by temporary modifications. Documents reviewed are listed in the attachment.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness (EP)

1EP2 Alert and Notification System (ANS)

a.

Inspection Scope (1 sample)

An onsite review was conducted to assess the maintenance and testing of PSEGs ANS.

During this inspection, the inspectors interviewed site EP staff responsible for implementation of the ANS testing and maintenance. Notifications pertaining to the ANS were reviewed for causes, trends, and corrective actions. The inspectors further discussed with PSEG the new ANS system design and its benefits over the previous system. The inspectors reviewed PSEGs original ANS design report to ensure compliance with those commitments for system maintenance and testing. The inspectors toured the Emergency Operations Facility (EOF). On March 28, 2007, the inspectors observed a silent test of the ANS. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP3 Emergency Response Organization (ERO) Staffing and Augmentation System

a.

Inspection Scope (1 sample)

A review of Salem/Hope Creeks ERO augmentation staffing requirements and the process for notifying the ERO was conducted. This was performed to ensure the readiness of key staff for responding to an event and to ensure timely facility activation.

The inspectors reviewed procedures, notifications, and call-in drills associated with the ERO notification system and drills. The inspectors interviewed personnel responsible for testing the ERO augmentation process. The inspectors compared qualification requirements to the training records for a sample of ERO members. The inspectors also verified that the EP department staff were receiving required training as specified in the emergency plan. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level (EAL) and Emergency Plan Changes

a.

Inspection Scope (1 sample)

Prior to this inspection, the NRC had received and acknowledged changes made to the Salem/Hope Creek Emergency Plan and implementing procedures. PSEG developed these changes in accordance with 10 CFR 50.54(q), and determined that the changes did not result in a decrease in effectiveness to the Plan. PSEG also determined that the plan continued to meet the requirements of 10 CFR 50.47(b) and 10 CFR 50 Appendix E.

During this inspection, the inspectors conducted a sampling review of Salem/Hope Creeks 10 CFR 50.54(q) screenings for the changes made to the Plan that could potentially result in a decrease in effectiveness. This review did not constitute NRC approval of the changes and, as such, the changes remain subject to future NRC inspection. Also, the NRC reviewed PSEGs EAL scheme for logic and consistency. The requirements in 10 CFR 50.54(q) were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses

a.

Inspection Scope (1 sample)

The inspectors reviewed EP self-assessments and audit reports to assess PSEGs ability to evaluate their performance and programs. The inspectors reviewed notifications initiated from December, 2005 to March, 2007 at Salem/Hope Creek from drills, self-assessments, and audits. Applicable emergency planning standards of 10 CFR 50.47 and the related requirements of 10 CFR 50, Appendix E were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

a.

Inspection Scope (1 sample)

Resident inspectors evaluated the conduct of a simulator examination scenario on January 20, 2007, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the simulated control room to verify that event classification and notifications were done in accordance with the Hope Creek Event Classification Guide. The inspectors also observed PSEGs critique of the examination to compare any inspector-observed weakness with those identified by PSEG personnel to verify whether PSEG was properly identifying weaknesses.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01) a.

Inspection Scope (7 samples)

The inspectors reviewed all PSEG performance indicators for the Occupational Radiation Safety Cornerstone for followup.

The inspectors identified exposure significant work areas within radiation areas, high radiation areas (<1 R/hr), or airborne radioactivity areas in the plant and reviewed associated PSEG controls and surveys of these areas to determine if controls (e.g.

surveys, postings, barricades) were acceptable.

The inspectors walked down these areas or their perimeters to determine: whether prescribed radiation work permits, procedure, and engineering controls were in place, whether PSEG surveys and postings were complete and accurate, and whether air samplers were properly located.

The inspectors examined PSEGs physical and programmatic controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools.

The inspectors discussed with the Radiation Protection Manager high dose rate - high radiation areas, and very high radiation areas (VHRA) controls and procedures. The inspectors verified that any changes to PSEG procedures do not substantially reduce the effectiveness and level of worker protection.

The inspectors discussed with first-line health physics supervisors the controls in place for special areas that have the potential to become VHRA during certain plant operations.

The inspectors reviewed and assessed the adequacy of PSEGs internal dose assessment for any actual internal exposure greater than 50 mrem committed effective dose equivalent (CEDE).

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02) a.

Inspection Scope (2 samples)

The inspectors reviewed the assumptions and basis for the current annual collective exposure estimate. The inspectors reviewed applicable procedures to determine the methodology for estimating work activity-specific exposures and the intended dose outcome.

The inspectors reviewed the exposure results and monitoring controls of declared pregnant workers. A total of six personnel were declared pregnant workers during 2006, with the maximum dose to an individual during the declaration period being 3 millirem.

b. Findings

No findings of significance were identified.

2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03)a.

Inspection Scope (1 sample)

The inspectors identified the types of portable radiation detection instrumentation used for job coverage of high radiation area work, other temporary area radiation monitors currently used in the plant, and continuous air monitors associated with jobs with the potential for workers to receive 50 mrem CEDE.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a.

Inspection Scope (6 samples)

Cornerstone: Initiating Events

The inspectors reviewed PSEGs program to gather, evaluate and report information on the following performance indicators (PIs). The inspectors used the guidance contained in (Nuclear Energy Institute) NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 4, to assess the accuracy of PSEGs collection and reporting of PI data. The documents reviewed by the inspectors are listed in the attachment.

C Unplanned SCRAMS per 7,000 Critical Hours C

Unplanned SCRAMS with Loss of Normal Heat Removal C

Unplanned Power Changes per 7,000 Critical Hours The inspectors verified the accuracy and completeness of reported manual and automatic unplanned scrams during the period of January 1, 2006 through December 31, 2006, for the Unplanned Scrams per 7,000 Critical Hours PI.

The inspectors reviewed and verified PSEGs basis for including or excluding any unplanned reactor scrams for the Unplanned Scrams with Loss of Normal Heat Removal PI during the period of January 1, 2006 through December 31, 2006.

The inspectors verified the accuracy and completeness of reported transients that resulted in unplanned changes in reactor power of greater than 20 percent power for the Unplanned Power Changes per 7,000 Critical Hours PI during the period of January 1, 2006 through December 31, 2006.

Cornerstone: Emergency Preparedness (3 samples)

C Drill and Exercise Performance C

ERO Drill Participation C

Alert and Notification System Reliability The inspectors reviewed supporting documentation from EP drills and ANS tests during the period of January 1, 2006 through December 31, 2006 to verify the accuracy of the reported data.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Review of Items Entered into the Corrective Action Program

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into PSEG's corrective action program. This was accomplished by reviewing the description of each new notification and attending daily management review committee meetings.

Documents reviewed are listed in the attachment.

.2 Annual Sample: Bailey Logic Module Failures

a.

Inspection Scope (1 sample)

The inspectors reviewed PSEGs actions to address an adverse trend in Bailey Logic Module failures. A number of issues have been identified in the PSEG corrective action program (CAP) describing a rising number of Bailey logic card failures. The issues were selected for review based on their potential to increase the likelihood of an initiating event or cause the inoperability of a safety system. The inspectors reviewed PSEG procedures, vendor documents, design change packages, notifications, orders, corrective actions, and apparent cause evaluations to understand the equipment functions and operational history, as well as the identification, evaluation, and corrective actions associated with the degraded conditions. System engineers, reactor operators and other PSEG staff were interviewed to gain additional insights on the failures.

The following examples illustrate a sampling of issues associated with Bailey Logic Module failures:

On August 25, 2006, a Bailey Logic Module failure resulted in automatic closure of a turbine auxiliaries cooling system (TACS) return isolation valve and an unplanned power reduction to 78% power. Operators manually isolated the B SACS loop then restored TACS cooling to stabilize the plant. Post-event review identified that the Field Programmable Logic Array chip in the Bailey Logic Module failed causing the automatic isolation of the valve. Corrective actions included replacement of the failed logic card, failure analysis of the faulty card, and continuation of the Bailey card replacement project.

On November 27, 2006, indication was lost for the D emergency diesel generator output breaker. Operators ordered the emergent replacement of the card even though they suspected the problem only impacted the indication portion of the Bailey Logic Module.

The post-replacement testing revealed that the failure would have prevented automatic and main control room operation of the diesel output breaker. Corrective actions included replacement of the failed logic card, a more detailed failure analysis of the faulty card, and re-evaluation of the Bailey card replacement project.

b. Findings

& Observations No findings of significance were identified.

The inspectors found that PSEG appropriately identified degraded conditions associated with Bailey Logic Module failures and entered them into the corrective action program.

Evaluations of degraded conditions were thorough, and included considerations for extent of condition. The inspectors reviewed the above examples and determined that performance deficiencies did not exist. Corrective actions developed by PSEG were appropriate to adequately address identified deficiencies.

4OA3 Event Followup

.1 Hope Creek Automatic Scram on January 29, 2007

a.

Inspection Scope (1 sample)

Hope Creek completed a scheduled maintenance outage on January 29, 2007, at 10:51 pm when the main generator was synchronized to the 500 kV grid. At 11:02 pm, control room operators observed reactor water level lower than expected and took action to restore level. Efforts to restore reactor water level were unsuccessful. At 11:10 pm, RPV water level was below 12.5 inches and the reactor protection system automatically inserted all control rods into the reactor core (a reactor scram).

The inspectors responded to the control room following the reactor scram to observe post-scram operations. The inspectors collected data from the plant computer to evaluate plant conditions prior to, during, and following the transient. The inspectors observed and participated in interviews with control room operators to gain an understanding of how operators responded to the transient. The inspectors observed engineering technical analysis and evaluation meetings and interviewed engineers to gain an understanding of the transient and to assess PSEGs evaluation process. The inspectors observed the Plant Oversight Review Committee meeting prior to plant startup to evaluate whether PSEG appropriately resolved the issues that led to the transient.

A root cause evaluation identified a failed reactor feed pump minimum flow valve as the cause of the level control problem and subsequent reactor scram. Corrective actions included repair of a reactor feed pump flow instrument tubing line and clarification to the low power operating portion of the feedwater system operating procedure. Documents reviewed are listed in the attachment.

b. Findings

No findings of significance were identified.

.2 (Closed) LER 05000354/2006-005-00, Drywell Hoist Breaker Not Open Prior to Mode 2

Entry On December 18, 2006, PSEG identified that breaker 52-263042 for the drywell safety relief valve (SRV) hoist was in the closed position. Technical Specification 3.8.4.1 requires that breaker 52-263042 be administratively maintained open in Operational Condition 1, 2, and 3. The breaker was not open and administratively controlled prior to entry into Operating Condition 2 on May 2, 2006. The inspectors reviewed the licensee event report (LER) and evaluations associated with the performance deficiency. The enforcement aspects of this finding are discussed in Section 4OA7. This LER is closed.

4OA5 Other Activities

.1 Independent Spent Fuel Storage Installation (ISFSI)

a.

Inspection Scope (1 sample)

The inspection was a follow-up to Inspection Report 05000354/2006010, completed on November 9, 2006. This inspection consisted of evaluating post dry cask storage activities associated with the recent completion of Hope Creeks initial ISFSI fuel loading campaign. Inspection activities consisted of interviews with cognizant personnel and reviews of PSEG documentation. Areas inspected included review of final dose totals for the initial ISFSI campaign, completed work packages, effectiveness of corrective actions implemented after loading of the first canister, PSEG identified lessons-learned during the initial campaign, ISFSI-related notifications, and verification of personnel training and qualifications.

The inspectors reviewed the completed work package for the loading of the first canister.

The work package included the procedures for loading and sealing the multi purpose canister (MPC), weld data sheets, liquid penetrant examination reports, and daily polar crane check lists. The inspectors verified that procedure steps were completed and necessary signatures and approvals obtained as required.

The inspectors interviewed cognizant personnel regarding the meaning and purpose of various signature completion steps in procedure NC.MD-PM.DCS-0003, Sealing, Drying, and Backfilling of a Loaded MPC. PSEG personnel confirmed that signatures for various steps signified that work was successfully completed and that associated data sheets had been reviewed by qualified individuals.

The inspectors discussed the training and qualification requirements for the Cask Loading Supervisor position with cognizant personnel. The inspectors determined that designated individuals were qualified as Cask Loading Supervisors in accordance with PSEGs program to meet the requirements of ANSI/ANS-3.1-1981, section 4.3.2. In addition these individuals were required to attend various training classes that included such topics as contract management, supplemental personnel oversight, and QA orientation. The inspectors observed that PSEG formally documented that individuals were properly qualified per ANSI/ANS-3.1, verified that the training database contained the documentation in the records for three individuals designated as Cask Loading Supervisors, and verified the required training for these individuals was maintained current.

The inspectors reviewed PSEG actions in response to exceeding the first fuel campaign dose estimate by approximately 1.5 rem. PSEG conducted a post-job critique after the first loading.

The inspectors reviewed PSEGs ISFSI-related corrective action notifications, lessons-learned documentation and action plans. Areas identified for evaluation included polar crane reliability improvements, dose reduction efforts, and transporter maintenance.

b. Findings

No findings of significance were identified.

.2 (Closed) URI 05000354/2006015-03, Inspection of PRA Quality Issues, and NRC Review

of Human Error Probability (HEP) Assigned Value for Battery Charger Cross-tie Operator Action The Senior Reactor Analyst (SRA) reviewed the unresolved item (URI) crediting operator action, NR-XTIE-CHARGE, in PSEGs probabilistic risk assessment (PRA) to determine if the model was reasonably representative of the as-built, as-operated nuclear power unit which it represents. This action is credited during postulated loss-of-offsite power (LOOP) events with an assumed concurrent failure of the B and D EDGs. Specifically, the Hope Creek PRA model credits manual operator actions to cross-tie power to the B or D battery chargers to provide power to the SRVs for reactor pressure control. For the NR-XTIE-CHARGE action to be successful, it must be completed prior to the depletion of the batteries. During the Component Design Bases Inspection, completed on December 7, 2006, the inspection team questioned the appropriateness of assigning a HEP of 0.6 when the performance shaping factors, such as training, availability of equipment and diagnosis were not favorable. An inappropriate assignment of an HEP could have an adverse impact on the ability of PSEG to assess and manage risk during normal plant operations.

The SRA conducted a sensitivity analysis for maintenance rule risk assessments which would be impacted by the NR-XTIE-CHARGE operator action. The most limiting maintenance configuration would be a HPCI system unavailability with B SACS in standby, D SSW pump in standby, B control rod drive pump in standby, and air compressor 10K107 in standby. A bounding unavailability of 14 days was assigned, which is the technical specification allowed outage time for HPCI. This was considered conservative because the 2002 - 2004 unavailability data from the Mitigating System Performance Index (MSPI) bases documents shows that the largest HPCI unavailability for this period occurred in July 2004 in which 154.23 hrs. (6.43 days). There were no significant outages of other monitored components during this period. Other MSPI components included in the sensitivity analysis were also reviewed and found to have a negligible impact. The HEP evaluated for the analysis ranged from PSEGs assigned value of 0.6 (60% chance of failure) to 1.0 (100% chance of failure). Utilizing the guidance provided in Inspection Manual Chapter (IMC) 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, the SRA concluded that under the most bounding assumptions, the changes in the maintenance rule risk assessment would not be significant and would be within the acceptable range of PRA uncertainty.

The generic issues associated with PRA quality are being addressed by the staff as outlined and updated in SECY-07-0042, Status of the Plan for the Implementation of the Commissions Phased Approach to Probabilistic Risk Assessment Quality, issued on March 7, 2007. The SRA concluded that the sensitivity of NR-XTIE-CHARGE did not impact the ability of PSEG to assess and manage risk during normal plant operations.

As such, for this issue it was determined that the model was reasonably representative of the as-built, as-operated nuclear power unit which it represents and this URI is closed.

4OA6 Meetings, Including Exit

On April 5, 2007, the inspectors presented their findings to members of PSEG management led by Messrs. Barnes and Perry. None of the information reviewed by the inspectors was considered proprietary.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by PSEG and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as Non-Cited Violations.

C Technical Specification 6.12.1 requires that access to, and activities in, each high radiation area be controlled by means of a radiation work permit. Entry into such areas shall be made only after dose rates in the area have been determined and entry personnel are knowledgeable of them. On December 12, 2006, a mechanical maintenance technician ascended into the Unit 1 turbine building crane cab, a posted high radiation area, without having been briefed or signed in on the appropriate high radiation area radiation work permit. The event is documented in PSEGs CAP as notification 20306791. The finding is only of very low safety significance because it did not involve a very high radiation area or personnel over-exposure.

C Technical Specification 3.8.4.1, "Primary Containment Penetration Conductor Overcurrent Protective Devices," requires that breaker 52-263042 for the drywell SRV hoist be administratively maintained open in Operational Conditions 1, 2, and 3. Contrary to this requirement, on December 18, 2006, PSEG identified that this breaker was closed. PSEG entered this issue into their corrective action program as notification 20307894. It was subsequently determined that the breaker had been closed since Hope Creek entered Operating Condition 2 on May 2, 2006. The issue was determined to be of very low safety significance, based on IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, because the finding does not represent an actual open pathway in the physical integrity of reactor containment.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

G. Barnes, Station Vice President
M. Massaro, Plant Manager
J. Perry, Plant Manager
D. Burgin, Emergency Preparedness Manager
D. Kelly, Radiation Protection Technical Support Manager
B. Sebastian, Radiation Protection Manager
B. Booth, Operations Director
R. Shindel, Senior Reactor Operator
E. Martin, Emergency Diesel Generators System Engineer
A. Bready, Contract Probabilistic Risk Assessment Engineer
M. Azzaro, License Requalification Instructor
B. Tyers, Building Equipment Drains System Engineer
D. Price, Manager Outage Services
M. Crisafulli, Mechanical Maintenance Superintendent
J. Louch, Manager Electrical Maintenance
J. Lewis, Project Manager Reactor
T. Wallender, Project Manager ISFSI
P. Marconni, Dry Cask Storage Loading Supervisor
J. Harris, ALARA Engineer
F. Foster, Operations Maintenance and Technical Instructor

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Opened/Closed

05000354/2006-005-00 LER Drywell Hoist Breaker Not Open Prior to Mode 2 Entry (Section 4OA3.2)

Closed

05000354/2006015-03 URI Inspection of PRA Quality Issues, and NRC Review of HEP Assigned Value for Battery Charger Cross-

tie Operator Action (Section 4OA5.2)

Discussed

None

LIST OF DOCUMENTS REVIEWED