IR 05000445/2018001

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NRC Integrated Inspection Report 05000445/2018001 and 05000446/2018001
ML18127A572
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 05/08/2018
From: Mark Haire
NRC/RGN-IV/DRP/RPB-A
To: Peters K
Vistra Operations Company
Haire M
References
IR 2018001
Download: ML18127A572 (25)


Text

May 8, 2018

SUBJECT:

COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000445/2018001 AND 05000446/2018001

Dear Mr. Peters:

On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 5, 2018, the NRC inspectors discussed the results of this inspection with Mr. Tom McCool, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented five findings of very low safety significance (Green) in this report.

All of these findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Comanche Peak Nuclear Power Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the Comanche Peak Nuclear Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Mark S. Haire, Chief Project Branch A Division of Reactor Projects

Docket Nos. 5000445 and 5000446 License Nos. NPF-87 and NPF-89

Enclosure:

Inspection Report 05000445/2017004 and 05000446/2017004 w/ Attachment:

Documents Reviewed

Enclosure U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000445, 05000446

License Numbers:

NPF-87, NPF-89

Report Numbers:

05000445/2018001 and 05000446/2018001

Enterprise Identifier: I-2018-001-0011

Licensee:

Vistra Operations Company, LLC

Facility:

Comanche Peak Nuclear Power Plant, Units 1 and 2

Location:

Glen Rose, Texas

Inspection Dates:

January 1, 2018 to March 31, 2018.

Inspectors:

J. Josey, Senior Resident Inspector

R. Kumana, Resident Inspector

I. Anchondo, Reactor Inspector

E. Uribe, Reactor Inspector

Approved By:

M. Haire, Chief

Project Branch A

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an Integrated Inspection at Comanche Peak Nuclear Power Plant in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations

Failure to Incorporate Design Information Into System Test Procedures Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-02; 05000446/2018001-02 Closed None 71152 -

Problem Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI,

Test Control, for the licensees failure to ensure that station test procedures incorporated all requirements contained in applicable design documents. Specifically, the stations test procedures for the component cooling water system failed to test the safeguards loops supply and return train isolation valves for leakage. Excess leakage from these valves could prevent the performance of a safety function. This finding was entered into the licensees corrective action program as Condition Report CR-2017-012024.

Failure to Follow Commercial Grade Dedication Process Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-01; 05000446/2018001-01 Closed None 7111112 -

Maintenance Effectiveness The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to accomplish activities affecting quality in accordance with documented procedures.

Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms to safety related without following the requirements of station procedure ECE-6.02-03, Critical Characteristics Development. The licensee entered this issue into the corrective action program as Condition Reports CR-CR-2016-009733 and CR-2017-007811.

Failure to Provide an Adequate Procedure Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-03; 05000446/2018001-03 Closed None 71152 -

Problem Identification and Resolution The inspectors identified a Green, non-cited violation of Technical Specification 5.4.1,

Procedures, associated with the licensees failure to provide procedures appropriate to the circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C Equipment, did not contain adequate instructions for wiring current to pressure (I/P)converters for safety related components which resulted in the steam generator atmospheric relief valve I/P converters being placed in a seismically unqualified configuration. This finding was entered into the licensees corrective action program as Condition Report CR-2017-011922.

Inadequate Maintenance Procedure for Feedwater Valves Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-04; 05000446/2018001-04 Closed None 71153 -

Follow-up of Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed Green, non-cited violation of Technical Specification 5.4.1, Procedures, associated with the licensees failure to prescribe adequate procedures for performing maintenance on the feedwater bypass control valves. Specifically, the licensees procedure failed to specify the correct torque on the handwheel screw locknut, resulting in a loose locknut which led to a control valve failure and a turbine trip. This finding was entered into the licensees corrective action program as Condition Report CR-2017-009139.

Failure to Correct a Significant Condition Adverse to Quality Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-05; 05000446/2018001-05 Closed P.2 - Problem Identification and Resolution,

Evaluation 71153-Follow-up of Events and Notices of Enforcement Discretion The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, associated with the licensees failure to take corrective action for the identified cause of a significant condition adverse to quality. Specifically, a feedwater bypass control valve vibrated open resulting in a turbine trip and initiation of auxiliary feedwater. The licensee determined that the cause was an inadequate procedure for performing maintenance on the feedwater bypass control valves, but failed to correct the inadequate procedure after identifying it as the cause of a control valve failure and a turbine trip. This finding was entered into the licensees corrective action program as Condition Report CR-2018-000959.

Additional Tracking Items

Type Issue number Title Report Section Status LER 05000445;05000446/

2017-001-00; 05000445;05000446/

2017-001-01 Unanalyzed Condition Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies 71153 Closed LER 05000446/2017-001-00; 05000446/2017-001-01; 05000446/2017-001-02 Auxiliary Feedwater System Actuation During Unit 2 Turbine Trip 71153 Closed LER 05000446/2017-002-00 Manual Reactor Trip Due to Dropped Rods 71153 Closed LER 05000446/2017-003-00 Manual Reactor Trip due to trip of both Main Feedwater Pumps 71153 Closed VIO 05000445/2015008-01; 05000446/2015008-01 Failure to Evaluate the Lack of Missile Protection on the Turbine Driven Auxiliary Feedwater Pumps Steam Exhaust Piping 92702 Closed

PLANT STATUS

Unit 1 began the inspection period at approximately 100 percent power, and operated at full power for the rest of the inspection period.

Unit 2 began the inspection period at approximately 100 percent power, and operated at full power for the rest of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather (1 Sample)

The inspectors evaluated readiness for impending adverse weather conditions for severe thunderstorms on March 19, 2018.

71111.04 - Equipment Alignment

Partial Walkdown (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 emergency diesel generator 2-01 while diesel generator 2-02 was out of service in an unplanned maintenance outage, on February 9, 2018
(2) Unit 2 Train B sequencer equipment during Train A actuation testing, on February 21, 2018
(3) Unit 1 coolant charging pump 1-02 while coolant charging pump 1-01 was out of service for maintenance, on March 21, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the Unit 1 emergency diesel generators system on March 14, 2018.

===71111.05AQFire Protection Annual/Quarterly

Quarterly Inspection===

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire zone SG10a, Unit 1 emergency diesel generator A, on March 23, 2018
(2) Fire zone SI12a, Unit 1 emergency diesel generator B, on March 23, 2018
(3) Fire zone SH11, Unit 1 emergency diesel generator A day tank room, on March 23, 2018
(4) Fire zone SJ13, Unit 1 emergency diesel generator B day tank room, on March 23, 2018
(5) Fire zone EM63, Unit 2 cable spreading room, on March 26, 2018

71111.06Flood Protection Measures Internal Flooding

The inspectors evaluated internal flooding mitigation protections in the Unit 2 emergency diesel generator rooms on March 14, 2018.

71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification

The inspectors observed and evaluated a crew during a simulator evaluated scenario for licensed operator requalification training on February 27, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated:

(1) Unit 1 control room actions during testing of steam generator atmospheric relief valves, on March 6, 2018
(2) Unit 1 control room operators response to the unexpected lifting of power operated relief valve 455A, on March 20, 2018

71111.12Maintenance Effectiveness Routine Maintenance Effectiveness

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Unit 1 emergency diesel generators, on March 6, 2018
(2) Unit 1 and Unit 2 steam generator atmospheric relief valves, on March 20, 2018

Quality Control (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:

(1) Unit 1 and Unit 2 upgrade of series 200 diaphragm seals

71111.13Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2 diesel generator 2-01 during unplanned maintenance on diesel 2-02, on January 11, 2018
(2) Unit 1 train A service water/component cooling water outage, on January 23, 2018
(3) Unit 2 component cooling water pump 2-02 recirculation flow control valve 2-HS-4537, on January 29, 2018
(4) Unit 2 emergent maintenance on diesel generator 2-02 due to broken amphenol, on February 7, 2018
(5) Unit 2 emergent maintenance on component cooling water pump 2-02 due to excessive shaft and bearing wear, on February 12, 2018

71111.15Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2, CR-2017-013643, 2-02 component cooling water heat exchange fouling, on January 8, 2018
(2) Unit 1 and 2, CR-2017-010346, condensate storage tank level transmitter uncertainty, on January 10, 2018
(3) Unit 1 and 2, IR-2018-000815, vent chiller X-04 liquid level too high, on January 30, 2018
(4) Unit 2, CR-2018-000941, component cooling water pump 2-02 excessive shaft wear, on February 9, 2018
(5) Unit 1, opening seismically qualified cabinet doors for maintenance, on February 15, 2018
(6) Unit 1, CR-2018-001264, water in-leakage degrading concrete, on March 1, 2018

71111.18Plant Modifications

The inspectors evaluated the following temporary or permanent modifications:

(1) Unit 2, component cooling water pump 2-02 increase in thrust bearing locknut torque due to identified degraded condition, on February 13, 2018

71111.19Post Maintenance Testing

The inspectors evaluated the following post maintenance tests:

(1) Unit 2, diesel generator 2-02 following corrective maintenance, on January 16, 2018
(2) Unit 2, diesel generator 2-02 following amphenol replacement, on February 9, 2018
(3) Unit 2, component cooling water pump 2-02 following corrective maintenance, on February 12, 2018
(4) Unit 2, centrifugal charging pump 2-01 following maintenance, on February 15, 2018
(5) Unit 2, steam generator 2-03 atmospheric relief valve following wiring removal, on March 18, 2018
(6) Unit 1, centrifugal charging pump 1-01 following maintenance, on March 28, 2018

===71111.22Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine===

(1) Unit 1, OPT-214A diesel generator 1-02, on January 12, 2018
(2) Unit 2, OPT-214B diesel generator 2-02, on March 12, 2018
(3) Unit 2, OPT-214B diesel generator 2-01, on March 22, 2018
(4) Unit 1, OPT-414A, blackout sequencer logic test, on March 29, 2018

In-service (2 Samples)

(1) Unit 2, OPT-208B, component cooling water pump 2-02 recirculation flow control valve 2-HS-4537, on January 30, 2018
(2) Unit 2, OPT-509, in-service testing of main steam isolation valves, on March 15, 2018

71114.06Drill Evaluation Emergency Planning Drill

The inspectors evaluated an extended loss of AC power to Unit 1 drill on February 14,

OTHER ACTIVITIES - BASELINE

71151Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below for the period from January 1 through December 31, 2017, for both Units 1 and 2:

(1) IE01: Unplanned Scrams per 7000 Critical Hours Sample
(2) IE03: Unplanned Power Changes per 7000 Critical Hours Sample
(3) IE04: Unplanned Scrams with Complications (USwC) Sample

71152Problem Identification and Resolution Annual Follow-up of Selected Issues

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Unexpected lifting of steam generator atmospheric relief valves 1-PV-2327 and 2-PV-2327
(2) Component cooling water supply cross connect valve leakage

71153Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports

The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) Licensee Event Report (LER) 05000445;05000446/2017-001-01, Unanalyzed Condition Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies, on January 11, 2017 [revisions 00 and 01 reviewed]
(2) LER 05000446/2017-001-02, Auxiliary Feedwater System Actuation During Unit 2 Turbine Trip, on August 11, 2017 [revisions 00, 01, and 02 reviewed]
(3) LER 05000446/2017-002-00, Manual Reactor Trip Due to Dropped Rods, on September 1, 2017
(4) LER 05000446/2017-003-00, Manual Reactor Trip due to trip of both Main Feedwater Pumps, on November 25,

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

92702Followup on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution Confirmatory Orders

The inspectors reviewed the licensees response to NOV 05000445/2015008-01; 05000446/2015008-01 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance will be achieved for this violation is adequately addressed and captured on the docket.

INSPECTION RESULTS

Failure to Follow Commercial Grade Dedication Process Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-01; 05000446/2018001-01 Closed None

71111.12 - Maintenance

Effectiveness The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to accomplish activities affecting quality in accordance with documented procedures.

Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms to safety related without following the requirements of station procedure ECE-6.02-03, Critical Characteristics Development.

Description:

While reviewing information related to Licensee Event Report 05000445;05000446/2017-001-01, Unanalyzed Condition Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies, inspectors reviewed the licensees root cause analyses documented in Condition Report CR-2016-010346. During this review inspectors noted that the licensee had upgraded previously installed commercial grade material to safety related. Specifically, Ashcroft series 200 diaphragms were supplied to the licensee during initial construction as non-safety related parts and installed in the centrifugal coolant charging pumps and positive displacement pumps suction and discharge pressure indicators as such. Subsequently, in 2003 the licensee determined that the diaphragm seals were in fact part of the safety related pressure boundary and were required to be safety related, and the licensee upgraded the Ashcroft series 200 diaphragms to safety related components due to seismic boundary concerns.

However, the inspectors also noted that the licensees root cause analyses stated that the upgrade of the diaphragm seal assemblies did not appear to have resulted in any additional evaluation. Inspectors questioned this and asked for the licensees commercial grade dedication packages for the Ashcroft series 200 diaphragms. The licensee responded that they had not done a commercial grade dedication package because the diaphragms had been supplied as quality group C (safety related) by the vendor. Inspectors asked to see the vendor paperwork designating the components as quality group C but the licensee responded that they did not have copies of this paperwork and they would have to get it from the vendor.

During subsequent discussions with the vendor, the licensee determine that the Ashcroft series 200 diaphragms were in fact provided as quality group C but this designation did not mean they were safety related. In fact, the vendor specification sheet provided to the licensee designated quality group C as non-safety related commercial grade components.

Based on this, the licensee determined that they had made errors in their assumptions when upgrading the diaphragms in 2003. Specifically, the licensee had made errors in their interpretation of what the vendor quality group designator meant, and they did not have copies of the appropriate specifications/paperwork when upgrading the diaphragm seal assemblies. The licensee initiated Condition Report CR-2016-009733 to capture this issue in the stations corrective action program. Subsequently, the licensee determined that there were approximately 29 additional Ashcroft series 200 diaphragms that had been inappropriately upgraded to safety related without commercial grade dedication packages.

Inspectors determined that had the licensee followed the requirements of station procedure ECE-6.02-03, Critical Characteristics Development, when upgrading the Ashcroft series 200 diaphragms to safety related components this would have required them to review all applicable paperwork. As such, inspectors determined that the licensees failure to follow procedural requirement resulted in non-safety related components being installed in a safety related application.

Corrective Action(s): The licensee performed an operability determination that established a reasonable expectation of operability pending additional corrective actions which include commercial grade dedication of the affected diaphragm seals.

Corrective Action Reference(s): CR-2016-009733 and CR-2017-007811

Performance Assessment:

Performance Deficiency: The licensees failure to follow the requirements of procedure ECE-6.02-03 when upgrading the safety classification of material was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the use of unqualified materials could result in equipment not being available to function during design events such as response to a seismic event.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At-Power, Exhibit 4, External Events Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because the finding is a deficiency affecting the design or qualification of a mitigating system, structure, or component (SSC), but the SSC maintained its operability.

Cross-cutting Aspect: The inspectors determined that the performance deficiency occurred more than three years ago and was not indicative of current performance.

Enforcement:

Violation: Title 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings, of a type appropriate to the circumstances. Procedure ECE-6.02-03, Critical Characteristics Development, an Appendix B quality related procedure, provides instructions for the commercial grade dedication of materials and parts.

Contrary to the above, in 2003 when upgrading the safety classification of Ashcroft series 200 diaphragms to safety related, the licensee failed to accomplish activities affecting quality in accordance with documented instructions, procedures, or drawings, of a type appropriate to the circumstances. Specifically, the licensee failed to follow the requirements of procedure ECE-6.02-03 when upgrading the safety classification of material.

Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Incorporate Design Information Into System Test Procedures Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-02; 05000446/2018001-02 Closed None

71152 - Problem

Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the licensees failure to ensure that station test procedures incorporated all requirements contained in applicable design documents. Specifically, the stations test procedures for the component cooling water system failed to test the safeguards loops supply and return train isolation valves for leakage. Excess leakage from these valves could prevent the performance of a safety function.

Description:

During fill and vent activities on the B train safeguards loop of the Unit 1 component cooling water system on October 24, 2017, the licensee noted a system pressure rise and determined the cause to be leakage past safeguards loops train A and B isolation valves 1-HV-4513 and 1-HV-4515 (respectively). The component cooling water system has four valves that close on an empty level in the surge tank to separate the safeguards loops from each other and from the non-safeguards loop. The licensee initiated Condition Report CR-2017-011897 to capture this issue in the stations corrective action program.

The inspectors reviewed this condition report and noted that the licensee had determined that the leakage past the valves was approximately 40.3 gallons per minute (gpm). Inspectors noted that this exceeded the allowable leakage limit of 37 gpm and the licensee had performed an operability determination and determined that the valves were operable but degraded based on an engineering evaluation. During their review of the operability evaluation, the inspectors noted the following:

  • Makeup to the surge tank is normally an automatic function; however, during events that result in a loss of instrument air, automatic makeup to the surge tank is lost and manual makeup is required but not assumed to start for 30 minutes following receipt of the empty alarm.
  • When the surge tank reaches the empty level setpoint, this causes safeguards loops supply and return train isolation valves 1-HV-4512, 1-HV-4514, 1-HV-4513, and 1-HV-4515 to close which separates the safeguards loops from each other and isolates them from the non-safeguards loop fast enough to prevent loss of inventory from at least one of the safeguards loops.
  • The surge tank design analysis assumes a system leak rate of 1 gpm (0.4 gpm for Unit 2).
  • Safeguards loop supply and return isolation valve design stroke time is 45 seconds.
  • Worst case break is in the non-seismic piping in the non-safeguards loop (seismic event will result in a loss of offsite power which stops automatic makeup to the surge tank).
  • Therefore, based on the operator response time and system leak rate the allowable train leakage limit is 37 gpm [10 gpm for Unit 2]. This ensures that there is adequate volume in the surge tank below the empty level to accommodate the water depletion due to postulated line break in the non-safeguard loop or the opposite train during the closing time of the isolation valves, without depleting the tank volume.
  • The licensee used measured stroke time of the valves, 27 seconds for both valves, as the assumed closing time and determined that the allowed train leakage was 46 gpm.

Inspectors also noted that previously the licensee had experienced a similar issue.

Specifically, on May 15, 2016, during train A restoration activities, the licensee identified that train A and B isolation valves 1-HV-4512 and 1-HV-4514 (respectively) were leaking by at approximately 43.55 gpm.

Inspectors questioned how the licensee was monitoring the system for leakage and queried the licensee about what testing is done on the system. The licensee responded that walk downs were done looking for leakage. Inspectors asked if the licensee performed train leakage test since the supply and return isolation valves were potential leak paths that could not be identified by walk down. The licensee responded that no testing looking for leaks was conducted, nor did the licensee believe they were required to do so.

However, following a review of the stations Updated Final Safety Analysis Report, Chapters 3 and 9, the inspectors determined that:

  • The component cooling water system and its safeguards loop components are required to withstand the effects of natural phenomena, such as seismic events, without loss of capability to perform its safety function [remove heat from safeguards loop components]. Therefore, one of the safeguards loops of the component cooling water system is required to remain operational during and following a failure of a non-seismic component in the non-safeguards loop following a seismic event assuming a single failure in the other loop [makes that loop unavailable].
  • The closure time of the safeguards loop isolation valves and the train leakage limit are design requirements since they affect the ability of the system to perform its safety function.

Further, Title 10 CFR 50, Appendix B, Criterion XI requires, in part, that a test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents.

Based on this, inspectors determined that the licensees practice of walking down the component cooling water system looking for leakage was not adequate and that the licensee should be testing the safeguards loops for leakage since leakage past the loop isolation valves could prevent the system from performing its safety function. Inspectors determined that this was applicable to both units.

Inspectors determined that this issue did not represent current performance because the licensee had not reviewed nor revised the testing methodology for the system in the last three years.

Corrective Action(s): The licensee performed an operability determination that established a reasonable expectation of operability pending development of additional corrective actions.

Corrective Action Reference(s): Condition Report CR-2017-012024

Performance Assessment:

Performance Deficiency: The licensees failure to incorporate design information into system test procedures was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, not monitoring for system leakage could result in a leak rate that would prevent the performance of system safety function.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At Power, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because:

(1) it was not a design deficiency;
(2) it did not represent a loss of system and/or function;
(3) it did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
(4) it did not result in the loss of a high safety significant nontechnical specification train.

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the performance deficiency was not reflective of current performance.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that a test program shall be established to assure that all testing required to demonstrate components will perform satisfactorily in service is identified and performed in accordance with written procedures which incorporate the requirements and acceptance limits contained in applicable design documents.

Contrary to the above, from initial construction until present, the licensee failed to established a test program to assure that all testing required to demonstrate components will perform satisfactorily in service is identified and performed in accordance with written procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Specifically, the licensee failed to incorporate design information into system test procedures for the component cooling water system relative to leak testing for the safeguards loops supply and return train isolation valves.

Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Provide Adequate Procedure Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-03; 05000446/2018001-03 Closed None

71152 - Problem

Identification and Resolution The inspectors identified a Green, non-cited violation of Technical Specification (TS) 5.4.1, Procedures, associated with the licensees failure to provide procedures appropriate to the circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C Equipment, did not contain adequate instructions for wiring current-to-pressure (I/P)converters for safety related components which resulted in the steam generator atmospheric relief valve I/P converters being placed in a seismically unqualified configuration.

Description:

On October 24, 2017, it was reported to the control room that steam generator 2-03 atmospheric dump valve 2-PV-2327 was leaking. The valve was found to be open approximately 20 percent. This issue was entered into the corrective action program as Condition Report CR-2017-011922. During the licensees investigation they noted that work had been going on in the vicinity of the I/P converter for valve 2-PV-2327 and that maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold pole. The licensee also found that the I/P converter output settings were high. When the licensee removed the cover of the converter they discovered that excess lead wires stored in the housing were in contact with moveable parts of the converter which caused valve 2-PV-2327 to open. The licensee moved the lead wires so they were no longer in contact with the moveable parts of the I/P converter.

Subsequently, on October 30, 2017, operators noted that steam generator 1-03 atmospheric dump valve 1-PV-2327 was not indicating fully shut as demanded. The valve was found to be open approximately 20 percent. This issue was entered into the corrective action program as Condition Report CR-2017-012141. During the licensees investigation they noted that work had been going on in the vicinity of the I/P converter for valve 1-PV-2327 and that maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold pole. The licensee also found that the I/P converter output settings were high. When the licensee removed the cover of the converter they discovered that excess lead wires stored in the housing were in contact with moveable parts of the converter which caused valve 1-PV-2327 to open. The licensee moved the lead wires so they were no longer in contact with the moveable parts of the I/P converter.

The licensee performed an equipment cause analysis checklist and determined that inadequate work practices was the cause of the issues. Inspectors questioned the licensees identified cause in that that both issues appeared to happen after the housing for the converters was struck with a scaffold pole, and raised concerns regarding seismic qualification of the converters.

These concerns were expressed to the licensee who subsequently determined that the excess wiring in the converter housing was not in a qualified seismic configuration. The licensee determined that this configuration had existed most likely since initial installation of the I/P converters and this was due to inadequate guidance provided in station procedure INC-2085, Rework and Replacement of I&C Equipment, for maintenance personnel regarding proper storage of excess field leads. Specifically, the procedure did not provide sufficient guidance to ensure that electrical lead wire or other components within the I/P converter were sufficiently secured to preclude contact with the moveable parts of the I/P converter, in order to ensure the function and seismic qualification of the components were maintained.

Corrective Action(s): The licensee performed an operability determination that established a reasonable expectation of operability, developed work orders to remove the excess wiring from the converters, and changed procedure INC-2085 to not allow excess wiring in the converter housing.

Corrective Action Reference(s): Condition Report CR-2017-011922

Performance Assessment:

Performance Deficiency: The licensees failure to prescribe adequate procedures to perform quality related activities associated with the steam generator atmospheric relief valve I/P converters was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the improper training of the lead wires resulted in the I/P converters being in a non-seismically qualified configuration.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding was of very low safety significance (Green)because:

(1) it was not a design deficiency;
(2) it did not represent a loss of system and/or function;
(3) it did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
(4) it did not result in the loss of a high safety significant non-technical specification train.

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the performance deficiency was not reflective of current performance.

Enforcement:

Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-related equipment be performed in accordance with written procedures appropriate to the circumstances.

Contrary to the above, from initial installation through March 13, 2018, for maintenance activities on steam generator atmospheric relief valve I/P converters, an activity that can affect the performance of safety-related equipment to which Technical Specification 5.4.1.a applies, the licensee failed to assure that the maintenance procedures were appropriate to the circumstances.

Disposition: This violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy.

Inadequate Maintenance Procedure for Feedwater Valves Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-04; 05000446/2018001-04 Closed None 71153 - Follow-up of Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, Green non-cited violation of TS 5.4.1, Procedures, associated with the licensees failure to prescribe adequate procedures for performing maintenance on the feedwater bypass control valves. Specifically, the licensees procedure failed to specify the correct torque on the hand wheel screw locknut, resulting in a loose locknut which led to a control valve failure and a turbine trip.

Description:

During the Unit 2 startup on August 11, 2017, following a forced outage, a turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main generator on the grid. The turbine trip and initiation of auxiliary feedwater was caused by steam generator 2-02 water level rising above the high level setpoint due to a failure of the steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand. These valves are equipped with a valve hand wheel locknut designed to prevent the manual hand wheel from rotating due to vibration. The valve failed to close because the valve hand wheel locknut had backed off its normal fully closed position allowing the manual hand wheel to rotate open and preventing the valve from closing. The licensee performed a review of work history on the valve and identified work activities during which the locknut was manipulated.

The licensee determined that the locknut was last manipulated during replacement of the 2-LV-2163 elastomers on October 15, 2015. The work was done in accordance with MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, Section 8.5. The guidance in MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN hand wheel screw locknut, but does not include specific acceptance criteria or guidance on the required torque to apply when tightening. For comparison, MSM-C0-6602 section 8.4 also includes a step to tighten the locknut, but states TIGHTEN hand wheel screw locknut snug tight. The phrase snug tight is used by licensee maintenance personnel to denote a qualitative torque value to apply to a component to ensure it will not come loose during normal operation. The licensee determined that the locknut needed to be left snug tight, and that the guidance in section 8.5 was not adequate. The inspectors determined that the inadequate procedural guidance had existed in the procedure since October 2007.

Inspectors determined that the failure of steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand was a significant condition adverse to quality because this issue resulted in a turbine trip and initiation of auxiliary feedwater, and could have resulted in a reactor scram

Corrective Action(s): The licensee verified all feedwater bypass control valve locknuts have been properly tightened in accordance with the appropriate qualitative torque value of snug tight.

Corrective Action Reference(s): CR-2017-009139

Performance Assessment:

Performance Deficiency: The licensees failure to prescribe adequate procedures to perform quality related activities associated with the feedwater bypass control valves was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the inadequate procedure resulted in a failure of a feedwater bypass control valve leading to an unplanned turbine trip and initiation of auxiliary feedwater.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition.

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the performance deficiency was not reflective of current performance.

Enforcement:

Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-related equipment be performed in accordance with written procedures appropriate to the circumstances.

Contrary to the above, from October 2007 through August 2017, for maintenance activities on the feedwater bypass control valves, an activity that can affect the performance of safety-related equipment to which Technical Specification 5.4.1.a applies, the licensee failed to assure that the maintenance procedures were appropriate to the circumstances.

Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Correct a Significant Condition Adverse to Quality Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-05; 05000446/2018001-05 Closed P.2 - Problem Identification and Resolution, Evaluation 71153 - Follow-up of Events and Notices of Enforcement Discretion The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, associated with the licensees failure to take corrective action to preclude repetition of a significant condition adverse to quality. Specifically, a feedwater bypass control valve vibrated open resulting in a turbine trip and initiation of auxiliary feedwater. The licensee determined that the cause was an inadequate procedure for performing maintenance on the feedwater bypass control valves, but failed to correct the inadequate procedure after identifying it as the cause of a control valve failure and a turbine trip.

Description:

During the Unit 2 startup on August 11, 2017, following a forced outage, a turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main generator on the grid (refer to NCV 05000445/2018001-04; 05000446/2018001-04 above).

The turbine trip and initiation of auxiliary feedwater was caused by steam generator 2-02 water level rising above the high level setpoint due to a failure of the steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand. Inspectors determined that this was a significant condition adverse to quality because this issue resulted in a turbine trip and initiation of auxiliary feedwater, and could have resulted in a reactor scram.

The licensee determined that the valve failed to close because the valve hand wheel locknut had backed off its normal fully closed position, preventing the valve from closing. The licensee performed a cause evaluation and identified that MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, contained inadequate guidance for restoration of the valve following maintenance. The guidance in MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN hand wheel screw locknut, but does not include specific acceptance criteria or guidance on the required torque to apply when tightening. Section 8.5 is used to perform elastomer replacement on these valves and was last used on 2-LV-2163 during replacement of the elastomers on October 15, 2015. Although the procedure contained inadequate guidance in section 8.5, the procedure also contains a section for general reassembly of the valve. MSM-C0-6602 section 8.4 includes a step to tighten the locknut, but states TIGHTEN hand wheel screw locknut snug tight. The phrase snug tight is used by licensee maintenance personnel to denote a qualitative torque value to apply to a component to ensure it will not come loose during normal operation. The licensee, in developing their corrective action plan, conflated section 8.4 and 8.5 and erroneously credited the correct step in section 8.4 as a corrective action for the inadequate step in section 8.5. The licensee assumed the corrective action had been completed during a procedural revision in 2012, and closed the corrective action plan without correcting section 8.5.

The inspectors reviewed the cause evaluation and corrective actions and identified that the licensee had failed to correct the inadequate procedure. The inspectors determined that MSM-C0-6602 section 8.5, step 8.5.43 was not revised, and no action was planned to revise it. The inspectors determined this to be a result of the licensees cause evaluation failing to identify the specific inadequate procedural step that caused the failure and as a result did not correct the deficiency.

The inspectors determined that the licensee had failed to implement corrective actions to preclude repetition of a significant condition adverse to quality.

Corrective Action(s): The licensee has verified all feedwater bypass control valve locknuts have been properly tightened, and changed procedure MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, step 8.5.43 to require the locknut to be tightened snug tight.

Corrective Action Reference(s): CR-2018-000959

Performance Assessment:

Performance Deficiency: The licensees failure to implement corrective actions to preclude repetition of a significant condition adverse to quality was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the inadequate procedure could reasonably be expected to result in another failure of the control valve and subsequent turbine trip.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition.

Cross-cutting Aspect: The finding was assigned a cross-cutting aspect of evaluation because the licensee did not thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. (P.2)

Enforcement:

Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that, for significant conditions adverse to quality, measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition.

Contrary to the above, from August 2017 through February 2018, the licensee failed to establish measures to assure corrective action was taken to preclude repetition of a significant condition adverse to quality. Specifically, the licensee failed to correct the cause of the event by correcting the inadequate maintenance procedure for the feedwater bypass control valves.

Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

The inspectors confirmed that proprietary information was controlled to protect from public disclosure.

On March 31, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. T. McCool, Site Vice President, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the inspection period.

DOCUMENTS REVIEWED

7111112 - Maintenance Effectiveness

Condition Reports

CR-2016-009733

CR-2017-007811

CR-2016-010346

CR-2016-008375

CR-2003-000664

Procedures

(Number)

Title

Revision

Or Date

ECE-6.02-03

Critical Characteristics Development

5b

71152 - Problem Identification and Resolution

Condition Reports

CR-2017-012024

CR-2017-011897

CR-2016-004715

CR-2017-011922

CR-2017-012141

CR-2017-012144

CR-2018-000909

CR-2017-011944

CR-2018-002058

CR-2018-001629

Work Orders

3793710

3505655

3793738

3-01-330488-02

3-01-330490-02

3-01-332709-01

3-01-330492-02

4793333

5516071

5435660

20265

20201

25302

20253

Procedures

(Number)

Title

Revision

Or Date

MSM-C0-8837

Fisher Butterfly Valve Rework

ICA-101

I&C Work Control

INC-2085

Rework and Replacement of I&C Equipment

INC-4270A

Channel Calibration Power Relief Valve Control

Steam Generator 3 Channel 2327

Miscellaneous Documents

Number

Title

Revision

or Date

ME(B)-073

CCW Surge Tank Volume

SEQSP-MS-78-01

Fisher Air Operated Globe Valve Model 8X6 EWP

71153 - Follow-up of Events and Notices of Enforcement Discretion

Condition Reports

CR-2017-009139

CR-2018-000959

CR-2013-006702

CR-2017-005448

Procedures

(Number)

Title

Revision

Or Date

MSM-C0-6602

Fisher Diaphragm Actuator Maintenance

K. Peters

COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT

05000445/2018001 AND 05000446/2018001 - DATED MAY 8, 2018

DISTRIBUTION

KKennedy, RA

SMorris, DRA

AVegel, DRP

MShaffer, DRS

JClark, DRS

RLantz, DRP

JJosey, DRP

RKumana, DRP

MHaire, DRP

RAlexander, DRP

LNewman, DRP

IAnchondo, DRS

DLackey, DRP

JBowen, RIV/OEDO

SKirkwood, RC

VDricks, ORA

JWeil, OCA

MOBanion, NRR

AMoreno, RIV/OCA

BMaier, RSLO

GGeorge, IPAT

EUribe, IPAT

MHerrera, DRMA

RIV ACES

ROP Reports

Electronic Distribution for Comanche Peak Nuclear Power Plant

OFFICIAL RECORD COPY

ADAMS ACCESSION NUMBER: ML18127A572

SUNSI Review

By: MSH/rdr

ADAMS

Yes No

Non-Sensitive

Sensitive

Publicly Available Keyword:

Non-Publicly Available NRC-002

OFFICE

SRI:DRP/A

RI:DRP/A

SPE:DRP/A

BC:EB1

BC:EB2

BC:OB

NAME

JJosey

RKumana

RAlexander

TFarnholtz

JDrake

VGaddy

SIGNATURE

/RA/

/RA/

/RA/

/RA/

/RA/

/RA/

DATE

04/30/18

04/30/18

04/27/18

04/26/18

04/26/18

04/26/18

OFFICE

RI:DRP/A

RI:DRP/A

BC:PSB2

TL-IPAT

BC:DRP/A

NAME

IAnchondo

EUribe

HGepford

GGeorge

MHaire

SIGNATURE

/RA/

/RA/

/RA/

/RA/

/RA/

DATE

04/26/2018

05/01/18

05/01/18

04/27/18

05/8/2018

May 8, 2018

Mr. Ken

J. Peters, Senior Vice President

and Chief Nuclear Officer

Vistra Operations Company LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT:

COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED

INSPECTION REPORT 05000445/2018001 AND 05000446/2018001

Dear Mr. Peters:

On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 5, 2018, the NRC

inspectors discussed the results of this inspection with Mr. Tom McCool, Site Vice President,

and other members of your staff. The results of this inspection are documented in the enclosed

report.

NRC inspectors documented five findings of very low safety significance (Green) in this report.

All of these findings involved violations of NRC requirements. The NRC is treating these

violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement

Policy.

If you contest the violations or significance of these NCVs, you should provide a response within

days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the

NRC resident inspector at the Comanche Peak Nuclear Power Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the

NRC resident inspector at the Comanche Peak Nuclear Power Plant.

K. Peters

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for

Withholding.

Sincerely,

/RA/

Mark

S. Haire, Chief

Project Branch A

Division of Reactor Projects

Docket Nos. 5000445 and 5000446

License Nos. NPF-87 and NPF-89

Enclosure:

Inspection Report 05000445/2017004

and 05000446/2017004

w/ Attachment:

Documents Reviewed

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000445, 05000446

License Numbers:

NPF-87, NPF-89

Report Numbers:

05000445/2018001 and 05000446/2018001

Enterprise Identifier: I-2018-001-0011

Licensee:

Vistra Operations Company, LLC

Facility:

Comanche Peak Nuclear Power Plant, Units 1 and 2

Location:

Glen Rose, Texas

Inspection Dates:

January 1, 2018 to March 31, 2018.

Inspectors:

J. Josey, Senior Resident Inspector
R. Kumana, Resident Inspector
I. Anchondo, Reactor Inspector
E. Uribe, Reactor Inspector

Approved By:

M. Haire, Chief

Project Branch A

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an Integrated Inspection at Comanche Peak Nuclear Power Plant in

accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs

program for overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and

violations being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations

Failure to Incorporate Design Information Into System Test Procedures

Cornerstone Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000445/2018001-02;

05000446/2018001-02

Closed

None

71152 -

Problem

Identification

and

Resolution

The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI,

Test Control, for the licensees failure to ensure that station test procedures incorporated all

requirements contained in applicable design documents. Specifically, the stations test

procedures for the component cooling water system failed to test the safeguards loops supply

and return train isolation valves for leakage. Excess leakage from these valves could prevent

the performance of a safety function. This finding was entered into the licensees corrective

action program as Condition Report CR-2017-012024.

Failure to Follow Commercial Grade Dedication Process

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000445/2018001-01;

05000446/2018001-01

Closed

None

7111112 -

Maintenance

Effectiveness

The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to

accomplish activities affecting quality in accordance with documented procedures.

Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms

to safety related without following the requirements of station procedure ECE-6.02-03, Critical

Characteristics Development. The licensee entered this issue into the corrective action

program as Condition Reports CR-CR-2016-009733 and CR-2017-007811.

Failure to Provide an Adequate Procedure

Cornerstone Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000445/2018001-03;

05000446/2018001-03

Closed

None

71152 -

Problem

Identification

and

Resolution

The inspectors identified a Green, non-cited violation of Technical Specification 5.4.1,

Procedures, associated with the licensees failure to provide procedures appropriate to the

circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C

Equipment, did not contain adequate instructions for wiring current to pressure (I/P)

converters for safety related components which resulted in the steam generator atmospheric

relief valve I/P converters being placed in a seismically unqualified configuration. This finding

was entered into the licensees corrective action program as Condition Report CR-2017-

011922.

Inadequate Maintenance Procedure for Feedwater Valves

Cornerstone Significance

Cross-cutting

Aspect

Report

Section

Initiating

Events

Green

NCV 05000445/2018001-04;

05000446/2018001-04

Closed

None

71153 -

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors reviewed a self-revealed Green, non-cited violation of Technical Specification 5.4.1, Procedures, associated with the licensees failure to prescribe adequate

procedures for performing maintenance on the feedwater bypass control valves. Specifically,

the licensees procedure failed to specify the correct torque on the handwheel screw locknut,

resulting in a loose locknut which led to a control valve failure and a turbine trip. This finding

was entered into the licensees corrective action program as Condition Report CR-2017-

009139.

Failure to Correct a Significant Condition Adverse to Quality

Cornerstone Significance

Cross-cutting

Aspect

Report

Section

Initiating

Events

Green

NCV 05000445/2018001-05;

05000446/2018001-05

Closed

P.2 - Problem

Identification

and

Resolution,

Evaluation

71153-

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, associated with the licensees failure to take corrective action for the

identified cause of a significant condition adverse to quality. Specifically, a feedwater bypass

control valve vibrated open resulting in a turbine trip and initiation of auxiliary feedwater. The

licensee determined that the cause was an inadequate procedure for performing maintenance

on the feedwater bypass control valves, but failed to correct the inadequate procedure after

identifying it as the cause of a control valve failure and a turbine trip. This finding was entered

into the licensees corrective action program as Condition Report CR-2018-000959.

Additional Tracking Items

Type

Issue number

Title

Report

Section

Status

LER

05000445;05000446/

2017-001-00;

05000445;05000446/

2017-001-01

Unanalyzed Condition Involving

Teflon Installed in Containment

Spray Pump Diaphragm Seal

Assemblies

71153

Closed

LER 05000446/2017-001-00;

05000446/2017-001-01;

05000446/2017-001-02

Auxiliary Feedwater System

Actuation During Unit 2 Turbine

Trip

71153

Closed

LER 05000446/2017-002-00

Manual Reactor Trip Due to

Dropped Rods

71153

Closed

LER 05000446/2017-003-00

Manual Reactor Trip due to trip

of both Main Feedwater Pumps

71153

Closed

VIO

05000445/2015008-01;

05000446/2015008-01

Failure to Evaluate the Lack of

Missile Protection on the

Turbine Driven Auxiliary

Feedwater Pumps Steam

Exhaust Piping

2702

Closed

PLANT STATUS

Unit 1 began the inspection period at approximately 100 percent power, and operated at full

power for the rest of the inspection period.

Unit 2 began the inspection period at approximately 100 percent power, and operated at full

power for the rest of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem

Identification and Resolution. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather (1 Sample)

The inspectors evaluated readiness for impending adverse weather conditions for severe

thunderstorms on March 19, 2018.

71111.04 - Equipment Alignment

Partial Walkdown (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 2 emergency diesel generator 2-01 while diesel generator 2-02 was out of service in

an unplanned maintenance outage, on February 9, 2018

(2) Unit 2 Train B sequencer equipment during Train A actuation testing, on

February 21, 2018

(3) Unit 1 coolant charging pump 1-02 while coolant charging pump 1-01 was out of service

for maintenance, on March 21, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the

Unit 1 emergency diesel generators system on March 14, 2018.

71111.05AQFire Protection Annual/Quarterly

Quarterly Inspection (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected

areas:

(1) Fire zone SG10a, Unit 1 emergency diesel generator A, on March 23, 2018

(2) Fire zone SI12a, Unit 1 emergency diesel generator B, on March 23, 2018

(3) Fire zone SH11, Unit 1 emergency diesel generator A day tank room, on March 23, 2018

(4) Fire zone SJ13, Unit 1 emergency diesel generator B day tank room, on March 23, 2018

(5) Fire zone EM63, Unit 2 cable spreading room, on March 26, 2018

71111.06Flood Protection Measures

Internal Flooding (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the Unit 2 emergency

diesel generator rooms on March 14, 2018.

71111.11Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

The inspectors observed and evaluated a crew during a simulator evaluated scenario for

licensed operator requalification training on February 27, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated:

(1) Unit 1 control room actions during testing of steam generator atmospheric relief valves,

on March 6, 2018

(2) Unit 1 control room operators response to the unexpected lifting of power operated relief

valve 455A, on March 20, 2018

71111.12Maintenance Effectiveness

Routine Maintenance Effectiveness (2 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated

with the following equipment and/or safety significant functions:

(1) Unit 1 emergency diesel generators, on March 6, 2018

(2) Unit 1 and Unit 2 steam generator atmospheric relief valves, on March 20, 2018

Quality Control (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the

following equipment performance issues:

(1) Unit 1 and Unit 2 upgrade of series 200 diaphragm seals

71111.13Maintenance Risk Assessments and Emergent Work Control (5 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent

work activities:

(1) Unit 2 diesel generator 2-01 during unplanned maintenance on diesel 2-02, on

January 11, 2018

(2) Unit 1 train A service water/component cooling water outage, on January 23, 2018

(3) Unit 2 component cooling water pump 2-02 recirculation flow control valve 2-HS-4537,

on January 29, 2018

(4) Unit 2 emergent maintenance on diesel generator 2-02 due to broken amphenol, on

February 7, 2018

(5) Unit 2 emergent maintenance on component cooling water pump 2-02 due to excessive

shaft and bearing wear, on February 12, 2018

71111.15Operability Determinations and Functionality Assessments (6 Samples)

The inspectors evaluated the following operability determinations and functionality

assessments:

(1) Unit 2, CR-2017-013643, 2-02 component cooling water heat exchange fouling, on

January 8, 2018

(2) Unit 1 and 2, CR-2017-010346, condensate storage tank level transmitter uncertainty,

on January 10, 2018

(3) Unit 1 and 2, IR-2018-000815, vent chiller X-04 liquid level too high, on

January 30, 2018

(4) Unit 2, CR-2018-000941, component cooling water pump 2-02 excessive shaft wear, on

February 9, 2018

(5) Unit 1, opening seismically qualified cabinet doors for maintenance, on

February 15, 2018

(6) Unit 1, CR-2018-001264, water in-leakage degrading concrete, on March 1, 2018

71111.18Plant Modifications (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Unit 2, component cooling water pump 2-02 increase in thrust bearing locknut torque

due to identified degraded condition, on February 13, 2018

71111.19Post Maintenance Testing (6 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Unit 2, diesel generator 2-02 following corrective maintenance, on January 16, 2018

(2) Unit 2, diesel generator 2-02 following amphenol replacement, on February 9, 2018

(3) Unit 2, component cooling water pump 2-02 following corrective maintenance, on

February 12, 2018

(4) Unit 2, centrifugal charging pump 2-01 following maintenance, on February 15, 2018

(5) Unit 2, steam generator 2-03 atmospheric relief valve following wiring removal, on

March 18, 2018

(6) Unit 1, centrifugal charging pump 1-01 following maintenance, on March 28, 2018

71111.22Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine (4 Samples)

(1) Unit 1, OPT-214A diesel generator 1-02, on January 12, 2018

(2) Unit 2, OPT-214B diesel generator 2-02, on March 12, 2018

(3) Unit 2, OPT-214B diesel generator 2-01, on March 22, 2018

(4) Unit 1, OPT-414A, blackout sequencer logic test, on March 29, 2018

In-service (2 Samples)

(1) Unit 2, OPT-208B, component cooling water pump 2-02 recirculation flow control

valve 2-HS-4537, on January 30, 2018

(2) Unit 2, OPT-509, in-service testing of main steam isolation valves, on March 15, 2018

71114.06Drill Evaluation

Emergency Planning Drill (1 Sample)

The inspectors evaluated an extended loss of AC power to Unit 1 drill on

February 14, 2018.

OTHER ACTIVITIES - BASELINE

71151Performance Indicator Verification (6 Samples)

The inspectors verified licensee performance indicators submittals listed below for the

period from January 1 through December 31, 2017, for both Units 1 and 2:

(1)

IE01: Unplanned Scrams per 7000 Critical Hours Sample

(2)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample

(3)

IE04: Unplanned Scrams with Complications (USwC) Sample

71152Problem Identification and Resolution

Annual Follow-up of Selected Issues (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1) Unexpected lifting of steam generator atmospheric relief valves 1-PV-2327

and 2-PV-2327

(2) Component cooling water supply cross connect valve leakage

71153Follow-up of Events and Notices of Enforcement Discretion

Licensee Event Reports (4 Samples)

The inspectors evaluated the following licensee event reports which can be accessed at

https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) Licensee Event Report (LER) 05000445;05000446/2017-001-01, Unanalyzed Condition

Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies, on

January 11, 2017 [revisions 00 and 01 reviewed]

(2) LER 05000446/2017-001-02, Auxiliary Feedwater System Actuation During Unit 2

Turbine Trip, on August 11, 2017 [revisions 00, 01, and 02 reviewed]

(3) LER 05000446/2017-002-00, Manual Reactor Trip Due to Dropped Rods, on

September 1, 2017

(4) LER 05000446/2017-003-00, Manual Reactor Trip due to trip of both Main Feedwater

Pumps, on November 25, 2017

OTHER ACTIVITIES - TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

2702Followup on Traditional Enforcement Actions Including Violations, Deviations,

Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution

Confirmatory Orders

The inspectors reviewed the licensees response to NOV 05000445/2015008-01;

05000446/2015008-01 and determined that the reason, corrective actions taken and

planned to address recurrence, and the date when full compliance will be achieved for this

violation is adequately addressed and captured on the docket.

INSPECTION RESULTS

Failure to Follow Commercial Grade Dedication Process

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000445/2018001-01;

05000446/2018001-01

Closed

None

71111.12 -

Maintenance

Effectiveness

The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to

accomplish activities affecting quality in accordance with documented procedures.

Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms

to safety related without following the requirements of station procedure ECE-6.02-03,

Critical Characteristics Development.

Description: While reviewing information related to Licensee Event Report

05000445;05000446/2017-001-01, Unanalyzed Condition Involving Teflon Installed in

Containment Spray Pump Diaphragm Seal Assemblies, inspectors reviewed the licensees

root cause analyses documented in Condition Report CR-2016-010346. During this review

inspectors noted that the licensee had upgraded previously installed commercial grade

material to safety related. Specifically, Ashcroft series 200 diaphragms were supplied to the

licensee during initial construction as non-safety related parts and installed in the centrifugal

coolant charging pumps and positive displacement pumps suction and discharge pressure

indicators as such. Subsequently, in 2003 the licensee determined that the diaphragm seals

were in fact part of the safety related pressure boundary and were required to be safety

related, and the licensee upgraded the Ashcroft series 200 diaphragms to safety related

components due to seismic boundary concerns.

However, the inspectors also noted that the licensees root cause analyses stated that the

upgrade of the diaphragm seal assemblies did not appear to have resulted in any additional

evaluation. Inspectors questioned this and asked for the licensees commercial grade

dedication packages for the Ashcroft series 200 diaphragms. The licensee responded that

they had not done a commercial grade dedication package because the diaphragms had

been supplied as quality group C (safety related) by the vendor. Inspectors asked to see the

vendor paperwork designating the components as quality group C but the licensee responded

that they did not have copies of this paperwork and they would have to get it from the vendor.

During subsequent discussions with the vendor, the licensee determine that the Ashcroft

series 200 diaphragms were in fact provided as quality group C but this designation did not

mean they were safety related. In fact, the vendor specification sheet provided to the

licensee designated quality group C as non-safety related commercial grade components.

Based on this, the licensee determined that they had made errors in their assumptions when

upgrading the diaphragms in 2003. Specifically, the licensee had made errors in their

interpretation of what the vendor quality group designator meant, and they did not have

copies of the appropriate specifications/paperwork when upgrading the diaphragm seal

assemblies. The licensee initiated Condition Report CR-2016-009733 to capture this issue in

the stations corrective action program. Subsequently, the licensee determined that there

were approximately 29 additional Ashcroft series 200 diaphragms that had been

inappropriately upgraded to safety related without commercial grade dedication packages.

Inspectors determined that had the licensee followed the requirements of station procedure

ECE-6.02-03, Critical Characteristics Development, when upgrading the Ashcroft series 200

diaphragms to safety related components this would have required them to review all

applicable paperwork. As such, inspectors determined that the licensees failure to follow

procedural requirement resulted in non-safety related components being installed in a safety

related application.

Corrective Action(s): The licensee performed an operability determination that established a

reasonable expectation of operability pending additional corrective actions which include

commercial grade dedication of the affected diaphragm seals.

Corrective Action Reference(s): CR-2016-009733 and CR-2017-007811

Performance Assessment:

Performance Deficiency: The licensees failure to follow the requirements of procedure

ECE-6.02-03 when upgrading the safety classification of material was a performance

deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the equipment performance attribute of the Mitigating Systems

Cornerstone and affected the cornerstone objective to ensure availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the use of unqualified materials could result in equipment not being available to

function during design events such as response to a seismic event.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,

2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination

Process for Findings At-Power, Exhibit 4, External Events Screening Questions, the

inspectors determined the finding was of very low safety significance (Green) because the

finding is a deficiency affecting the design or qualification of a mitigating system, structure, or

component (SSC), but the SSC maintained its operability.

Cross-cutting Aspect: The inspectors determined that the performance deficiency occurred

more than three years ago and was not indicative of current performance.

Enforcement:

Violation: Title 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality shall be accomplished in

accordance with documented instructions, procedures, or drawings, of a type appropriate to

the circumstances. Procedure ECE-6.02-03, Critical Characteristics Development, an

Appendix B quality related procedure, provides instructions for the commercial grade

dedication of materials and parts.

Contrary to the above, in 2003 when upgrading the safety classification of Ashcroft series 200

diaphragms to safety related, the licensee failed to accomplish activities affecting quality in

accordance with documented instructions, procedures, or drawings, of a type appropriate to

the circumstances. Specifically, the licensee failed to follow the requirements of procedure

ECE-6.02-03 when upgrading the safety classification of material.

Disposition: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Failure to Incorporate Design Information Into System Test Procedures

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000445/2018001-02;

05000446/2018001-02

Closed

None

71152 -

Problem

Identification

and

Resolution

The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI,

Test Control, for the licensees failure to ensure that station test procedures incorporated all

requirements contained in applicable design documents. Specifically, the stations test

procedures for the component cooling water system failed to test the safeguards loops supply

and return train isolation valves for leakage. Excess leakage from these valves could prevent

the performance of a safety function.

Description: During fill and vent activities on the B train safeguards loop of the Unit 1

component cooling water system on October 24, 2017, the licensee noted a system pressure

rise and determined the cause to be leakage past safeguards loops train A and B isolation

valves 1-HV-4513 and 1-HV-4515 (respectively). The component cooling water system has

four valves that close on an empty level in the surge tank to separate the safeguards loops

from each other and from the non-safeguards loop. The licensee initiated Condition Report

CR-2017-011897 to capture this issue in the stations corrective action program.

The inspectors reviewed this condition report and noted that the licensee had determined that

the leakage past the valves was approximately 40.3 gallons per minute (gpm). Inspectors

noted that this exceeded the allowable leakage limit of 37 gpm and the licensee had

performed an operability determination and determined that the valves were operable but

degraded based on an engineering evaluation. During their review of the operability

evaluation, the inspectors noted the following:

Makeup to the surge tank is normally an automatic function; however, during events

that result in a loss of instrument air, automatic makeup to the surge tank is lost and

manual makeup is required but not assumed to start for 30 minutes following receipt of

the empty alarm.

When the surge tank reaches the empty level setpoint, this causes safeguards

loops supply and return train isolation valves 1-HV-4512, 1-HV-4514, 1-HV-4513,

and 1-HV-4515 to close which separates the safeguards loops from each other

and isolates them from the non-safeguards loop fast enough to prevent loss of

inventory from at least one of the safeguards loops.

The surge tank design analysis assumes a system leak rate of 1 gpm (0.4 gpm for

Unit 2).

Safeguards loop supply and return isolation valve design stroke time is 45 seconds.

Worst case break is in the non-seismic piping in the non-safeguards loop (seismic

event will result in a loss of offsite power which stops automatic makeup to the surge

tank).

Therefore, based on the operator response time and system leak rate the allowable

train leakage limit is 37 gpm [10 gpm for Unit 2]. This ensures that there is adequate

volume in the surge tank below the empty level to accommodate the water

depletion due to postulated line break in the non-safeguard loop or the opposite

train during the closing time of the isolation valves, without depleting the tank

volume.

The licensee used measured stroke time of the valves, 27 seconds for both valves, as

the assumed closing time and determined that the allowed train leakage was 46 gpm.

Inspectors also noted that previously the licensee had experienced a similar issue.

Specifically, on May 15, 2016, during train A restoration activities, the licensee identified that

train A and B isolation valves 1-HV-4512 and 1-HV-4514 (respectively) were leaking by at

approximately 43.55 gpm.

Inspectors questioned how the licensee was monitoring the system for leakage and queried

the licensee about what testing is done on the system. The licensee responded that walk

downs were done looking for leakage. Inspectors asked if the licensee performed train

leakage test since the supply and return isolation valves were potential leak paths that could

not be identified by walk down. The licensee responded that no testing looking for leaks was

conducted, nor did the licensee believe they were required to do so.

However, following a review of the stations Updated Final Safety Analysis Report, Chapters 3

and 9, the inspectors determined that:

The component cooling water system and its safeguards loop components are

required to withstand the effects of natural phenomena, such as seismic events,

without loss of capability to perform its safety function [remove heat from safeguards

loop components]. Therefore, one of the safeguards loops of the component cooling

water system is required to remain operational during and following a failure of a

non-seismic component in the non-safeguards loop following a seismic event

assuming a single failure in the other loop [makes that loop unavailable].

The closure time of the safeguards loop isolation valves and the train leakage limit

are design requirements since they affect the ability of the system to perform its

safety function.

Further, Title 10 CFR 50, Appendix B, Criterion XI requires, in part, that a test program shall

be established to assure that all testing required to demonstrate that structures, systems, and

components will perform satisfactorily in service is identified and performed in accordance

with written test procedures which incorporate the requirements and acceptance limits

contained in applicable design documents.

Based on this, inspectors determined that the licensees practice of walking down the

component cooling water system looking for leakage was not adequate and that the licensee

should be testing the safeguards loops for leakage since leakage past the loop isolation

valves could prevent the system from performing its safety function. Inspectors determined

that this was applicable to both units.

Inspectors determined that this issue did not represent current performance because the

licensee had not reviewed nor revised the testing methodology for the system in the last three

years.

Corrective Action(s): The licensee performed an operability determination that established a

reasonable expectation of operability pending development of additional corrective actions.

Corrective Action Reference(s): Condition Report CR-2017-012024

Performance Assessment:

Performance Deficiency: The licensees failure to incorporate design information into system

test procedures was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the equipment performance attribute of the Mitigating Systems

cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, not monitoring for system leakage could result in a leak rate that

would prevent the performance of system safety function.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,

2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination

Process for Findings At Power, Exhibit 2, Mitigating Systems Screening Questions, the

inspectors determined the finding was of very low safety significance (Green) because: (1) it

was not a design deficiency; (2) it did not represent a loss of system and/or function; (3) it did

not represent an actual loss of function of at least a single train for longer than its technical

specification allowed outage time; and (4) it did not result in the loss of a high safety

significant nontechnical specification train.

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the

performance deficiency was not reflective of current performance.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that

a test program shall be established to assure that all testing required to demonstrate

components will perform satisfactorily in service is identified and performed in accordance

with written procedures which incorporate the requirements and acceptance limits contained

in applicable design documents.

Contrary to the above, from initial construction until present, the licensee failed to established

a test program to assure that all testing required to demonstrate components will perform

satisfactorily in service is identified and performed in accordance with written procedures

which incorporate the requirements and acceptance limits contained in applicable design

documents. Specifically, the licensee failed to incorporate design information into system test

procedures for the component cooling water system relative to leak testing for the safeguards

loops supply and return train isolation valves.

Disposition: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Failure to Provide Adequate Procedure

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000445/2018001-03;

05000446/2018001-03

Closed

None

71152 -

Problem

Identification

and

Resolution

The inspectors identified a Green, non-cited violation of Technical Specification (TS) 5.4.1,

Procedures, associated with the licensees failure to provide procedures appropriate to the

circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C

Equipment, did not contain adequate instructions for wiring current-to-pressure (I/P)

converters for safety related components which resulted in the steam generator atmospheric

relief valve I/P converters being placed in a seismically unqualified configuration.

Description: On October 24, 2017, it was reported to the control room that steam generator

2-03 atmospheric dump valve 2-PV-2327 was leaking. The valve was found to be open

approximately 20 percent. This issue was entered into the corrective action program as

Condition Report CR-2017-011922. During the licensees investigation they noted that work

had been going on in the vicinity of the I/P converter for valve 2-PV-2327 and that

maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold

pole. The licensee also found that the I/P converter output settings were high. When the

licensee removed the cover of the converter they discovered that excess lead wires stored in

the housing were in contact with moveable parts of the converter which caused valve 2-PV-

27 to open. The licensee moved the lead wires so they were no longer in contact with the

moveable parts of the I/P converter.

Subsequently, on October 30, 2017, operators noted that steam generator 1-03 atmospheric

dump valve 1-PV-2327 was not indicating fully shut as demanded. The valve was found to be

open approximately 20 percent. This issue was entered into the corrective action program as

Condition Report CR-2017-012141. During the licensees investigation they noted that work

had been going on in the vicinity of the I/P converter for valve 1-PV-2327 and that

maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold

pole. The licensee also found that the I/P converter output settings were high. When the

licensee removed the cover of the converter they discovered that excess lead wires stored in

the housing were in contact with moveable parts of the converter which caused

valve 1-PV-2327 to open. The licensee moved the lead wires so they were no longer in

contact with the moveable parts of the I/P converter.

The licensee performed an equipment cause analysis checklist and determined that

inadequate work practices was the cause of the issues. Inspectors questioned the licensees

identified cause in that that both issues appeared to happen after the housing for the

converters was struck with a scaffold pole, and raised concerns regarding seismic

qualification of the converters.

These concerns were expressed to the licensee who subsequently determined that the

excess wiring in the converter housing was not in a qualified seismic configuration. The

licensee determined that this configuration had existed most likely since initial installation of

the I/P converters and this was due to inadequate guidance provided in station procedure

INC-2085, Rework and Replacement of I&C Equipment, for maintenance personnel

regarding proper storage of excess field leads. Specifically, the procedure did not provide

sufficient guidance to ensure that electrical lead wire or other components within the I/P

converter were sufficiently secured to preclude contact with the moveable parts of the I/P

converter, in order to ensure the function and seismic qualification of the components were

maintained.

Corrective Action(s): The licensee performed an operability determination that established a

reasonable expectation of operability, developed work orders to remove the excess wiring

from the converters, and changed procedure INC-2085 to not allow excess wiring in the

converter housing.

Corrective Action Reference(s): Condition Report CR-2017-011922

Performance Assessment:

Performance Deficiency: The licensees failure to prescribe adequate procedures to perform

quality related activities associated with the steam generator atmospheric relief valve I/P

converters was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the equipment performance attribute of the Mitigating Systems

cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the improper training of the lead wires resulted in the I/P

converters being in a non-seismically qualified configuration.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated

October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance

Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening

Questions, the inspectors determined the finding was of very low safety significance (Green)

because: (1) it was not a design deficiency; (2) it did not represent a loss of system and/or

function; (3) it did not represent an actual loss of function of at least a single train for longer

than its technical specification allowed outage time; and (4) it did not result in the loss of a

high safety significant non-technical specification train.

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the

performance deficiency was not reflective of current performance.

Enforcement:

Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be

established, implemented, and maintained covering the applicable procedures recommended

in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33,

Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-

related equipment be performed in accordance with written procedures appropriate to the

circumstances.

Contrary to the above, from initial installation through March 13, 2018, for maintenance

activities on steam generator atmospheric relief valve I/P converters, an activity that can

affect the performance of safety-related equipment to which Technical Specification 5.4.1.a

applies, the licensee failed to assure that the maintenance procedures were appropriate to

the circumstances.

Disposition: This violation is being treated as a Non-Cited Violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Inadequate Maintenance Procedure for Feedwater Valves

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000445/2018001-04;

05000446/2018001-04

Closed

None

71153 -

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors reviewed a self-revealed, Green non-cited violation of TS 5.4.1, Procedures,

associated with the licensees failure to prescribe adequate procedures for performing

maintenance on the feedwater bypass control valves. Specifically, the licensees procedure

failed to specify the correct torque on the hand wheel screw locknut, resulting in a loose

locknut which led to a control valve failure and a turbine trip.

Description: During the Unit 2 startup on August 11, 2017, following a forced outage, a

turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main

generator on the grid. The turbine trip and initiation of auxiliary feedwater was caused by

steam generator 2-02 water level rising above the high level setpoint due to a failure of the

steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand. These

valves are equipped with a valve hand wheel locknut designed to prevent the manual hand

wheel from rotating due to vibration. The valve failed to close because the valve hand wheel

locknut had backed off its normal fully closed position allowing the manual hand wheel to

rotate open and preventing the valve from closing. The licensee performed a review of work

history on the valve and identified work activities during which the locknut was manipulated.

The licensee determined that the locknut was last manipulated during replacement of the

2-LV-2163 elastomers on October 15, 2015. The work was done in accordance with

MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, Section 8.5. The guidance in

MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN hand wheel screw locknut, but

does not include specific acceptance criteria or guidance on the required torque to apply

when tightening. For comparison, MSM-C0-6602 section 8.4 also includes a step to tighten

the locknut, but states TIGHTEN hand wheel screw locknut snug tight. The phrase snug

tight is used by licensee maintenance personnel to denote a qualitative torque value to apply

to a component to ensure it will not come loose during normal operation. The licensee

determined that the locknut needed to be left snug tight, and that the guidance in section 8.5

was not adequate. The inspectors determined that the inadequate procedural guidance had

existed in the procedure since October 2007.

Inspectors determined that the failure of steam generator 2-02 feedwater bypass control

valve 2-LV-2163 to close on demand was a significant condition adverse to quality because

this issue resulted in a turbine trip and initiation of auxiliary feedwater, and could have

resulted in a reactor scram

Corrective Action(s): The licensee verified all feedwater bypass control valve locknuts have

been properly tightened in accordance with the appropriate qualitative torque value of snug

tight.

Corrective Action Reference(s): CR-2017-009139

Performance Assessment:

Performance Deficiency: The licensees failure to prescribe adequate procedures to perform

quality related activities associated with the feedwater bypass control valves was a

performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the procedure quality attribute of the Initiating Events

Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset

plant stability and challenge critical safety functions during shutdown as well as power

operations. Specifically, the inadequate procedure resulted in a failure of a feedwater bypass

control valve leading to an unplanned turbine trip and initiation of auxiliary feedwater.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,

2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events

Screening Questions, the inspectors determined the finding was of very low safety

significance (Green) because it did not cause a reactor trip and the loss of mitigation

equipment relied upon to transition the plant to a stable shutdown condition.

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the

performance deficiency was not reflective of current performance.

Enforcement:

Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be

established, implemented, and maintained covering the applicable procedures recommended

in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33,

Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-

related equipment be performed in accordance with written procedures appropriate to the

circumstances.

Contrary to the above, from October 2007 through August 2017, for maintenance activities on

the feedwater bypass control valves, an activity that can affect the performance of safety-

related equipment to which Technical Specification 5.4.1.a applies, the licensee failed to

assure that the maintenance procedures were appropriate to the circumstances.

Disposition: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Failure to Correct a Significant Condition Adverse to Quality

Cornerstone

Significance

Cross-cutting

Aspect

Report

Section

Initiating Events

Green

NCV 05000445/2018001-05;

05000446/2018001-05

Closed

P.2 - Problem

Identification

and Resolution,

Evaluation

71153 -

Follow-up of

Events and

Notices of

Enforcement

Discretion

The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B,

Criterion XVI, Corrective Action, associated with the licensees failure to take corrective

action to preclude repetition of a significant condition adverse to quality. Specifically, a

feedwater bypass control valve vibrated open resulting in a turbine trip and initiation of

auxiliary feedwater. The licensee determined that the cause was an inadequate procedure

for performing maintenance on the feedwater bypass control valves, but failed to correct the

inadequate procedure after identifying it as the cause of a control valve failure and a turbine

trip.

Description: During the Unit 2 startup on August 11, 2017, following a forced outage, a

turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main

generator on the grid (refer to NCV 05000445/2018001-04; 05000446/2018001-04 above).

The turbine trip and initiation of auxiliary feedwater was caused by steam generator 2-02

water level rising above the high level setpoint due to a failure of the steam generator 2-02

feedwater bypass control valve 2-LV-2163 to close on demand. Inspectors determined that

this was a significant condition adverse to quality because this issue resulted in a turbine trip

and initiation of auxiliary feedwater, and could have resulted in a reactor scram.

The licensee determined that the valve failed to close because the valve hand wheel locknut

had backed off its normal fully closed position, preventing the valve from closing. The

licensee performed a cause evaluation and identified that MSM-C0-6602, Fisher Diaphragm

Actuator Maintenance, contained inadequate guidance for restoration of the valve following

maintenance. The guidance in MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN

hand wheel screw locknut, but does not include specific acceptance criteria or guidance on

the required torque to apply when tightening. Section 8.5 is used to perform elastomer

replacement on these valves and was last used on 2-LV-2163 during replacement of the

elastomers on October 15, 2015. Although the procedure contained inadequate guidance in

section 8.5, the procedure also contains a section for general reassembly of the valve. MSM-

C0-6602 section 8.4 includes a step to tighten the locknut, but states TIGHTEN hand wheel

screw locknut snug tight. The phrase snug tight is used by licensee maintenance

personnel to denote a qualitative torque value to apply to a component to ensure it will not

come loose during normal operation. The licensee, in developing their corrective action plan,

conflated section 8.4 and 8.5 and erroneously credited the correct step in section 8.4 as a

corrective action for the inadequate step in section 8.5. The licensee assumed the corrective

action had been completed during a procedural revision in 2012, and closed the corrective

action plan without correcting section 8.5.

The inspectors reviewed the cause evaluation and corrective actions and identified that the

licensee had failed to correct the inadequate procedure. The inspectors determined that

MSM-C0-6602 section 8.5, step 8.5.43 was not revised, and no action was planned to revise

it. The inspectors determined this to be a result of the licensees cause evaluation failing to

identify the specific inadequate procedural step that caused the failure and as a result did not

correct the deficiency.

The inspectors determined that the licensee had failed to implement corrective actions to

preclude repetition of a significant condition adverse to quality.

Corrective Action(s): The licensee has verified all feedwater bypass control valve locknuts

have been properly tightened, and changed procedure MSM-C0-6602, Fisher Diaphragm

Actuator Maintenance, step 8.5.43 to require the locknut to be tightened snug tight.

Corrective Action Reference(s): CR-2018-000959

Performance Assessment:

Performance Deficiency: The licensees failure to implement corrective actions to preclude

repetition of a significant condition adverse to quality was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it adversely affected the procedure quality attribute of the Initiating Events

Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset

plant stability and challenge critical safety functions during shutdown as well as power

operations. Specifically, the inadequate procedure could reasonably be expected to result in

another failure of the control valve and subsequent turbine trip.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,

2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events

Screening Questions, the inspectors determined the finding was of very low safety

significance (Green) because it did not cause a reactor trip and the loss of mitigation

equipment relied upon to transition the plant to a stable shutdown condition.

Cross-cutting Aspect: The finding was assigned a cross-cutting aspect of evaluation because

the licensee did not thoroughly evaluate issues to ensure that resolutions address causes and

extent of conditions commensurate with their safety significance. (P.2)

Enforcement:

Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that,

for significant conditions adverse to quality, measures shall assure that the cause of the

condition is determined and corrective action taken to preclude repetition.

Contrary to the above, from August 2017 through February 2018, the licensee failed to

establish measures to assure corrective action was taken to preclude repetition of a

significant condition adverse to quality. Specifically, the licensee failed to correct the cause of

the event by correcting the inadequate maintenance procedure for the feedwater bypass

control valves.

Disposition: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

The inspectors confirmed that proprietary information was controlled to protect from public

disclosure.

On March 31, 2018, the inspectors presented the quarterly resident inspector inspection results

to Mr.

T. McCool, Site Vice President, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the

inspection period.

DOCUMENTS REVIEWED

7111112 - Maintenance Effectiveness

Condition Reports

CR-2016-009733

CR-2017-007811

CR-2016-010346

CR-2016-008375

CR-2003-000664

Procedures

(Number)

Title

Revision

Or Date

ECE-6.02-03

Critical Characteristics Development

5b

71152 - Problem Identification and Resolution

Condition Reports

CR-2017-012024

CR-2017-011897

CR-2016-004715

CR-2017-011922

CR-2017-012141

CR-2017-012144

CR-2018-000909

CR-2017-011944

CR-2018-002058

CR-2018-001629

Work Orders

3793710

3505655

3793738

3-01-330488-02

3-01-330490-02

3-01-332709-01

3-01-330492-02

4793333

5516071

5435660

20265

20201

25302

20253

Procedures

(Number)

Title

Revision

Or Date

MSM-C0-8837

Fisher Butterfly Valve Rework

ICA-101

I&C Work Control

INC-2085

Rework and Replacement of I&C Equipment

INC-4270A

Channel Calibration Power Relief Valve Control

Steam Generator 3 Channel 2327

Miscellaneous Documents

Number

Title

Revision

or Date

ME(B)-073

CCW Surge Tank Volume

SEQSP-MS-78-01

Fisher Air Operated Globe Valve Model 8X6 EWP

71153 - Follow-up of Events and Notices of Enforcement Discretion

Condition Reports

CR-2017-009139

CR-2018-000959

CR-2013-006702

CR-2017-005448

Procedures

(Number)

Title

Revision

Or Date

MSM-C0-6602

Fisher Diaphragm Actuator Maintenance

4