IR 05000445/2018001
| ML18127A572 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 05/08/2018 |
| From: | Mark Haire NRC/RGN-IV/DRP/RPB-A |
| To: | Peters K Vistra Operations Company |
| Haire M | |
| References | |
| IR 2018001 | |
| Download: ML18127A572 (25) | |
Text
May 8, 2018
SUBJECT:
COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000445/2018001 AND 05000446/2018001
Dear Mr. Peters:
On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 5, 2018, the NRC inspectors discussed the results of this inspection with Mr. Tom McCool, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented five findings of very low safety significance (Green) in this report.
All of these findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Comanche Peak Nuclear Power Plant.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the Comanche Peak Nuclear Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Mark S. Haire, Chief Project Branch A Division of Reactor Projects
Docket Nos. 5000445 and 5000446 License Nos. NPF-87 and NPF-89
Enclosure:
Inspection Report 05000445/2017004 and 05000446/2017004 w/ Attachment:
Documents Reviewed
Enclosure U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Docket Numbers:
05000445, 05000446
License Numbers:
Report Numbers:
05000445/2018001 and 05000446/2018001
Enterprise Identifier: I-2018-001-0011
Licensee:
Vistra Operations Company, LLC
Facility:
Comanche Peak Nuclear Power Plant, Units 1 and 2
Location:
Glen Rose, Texas
Inspection Dates:
January 1, 2018 to March 31, 2018.
Inspectors:
J. Josey, Senior Resident Inspector
R. Kumana, Resident Inspector
I. Anchondo, Reactor Inspector
E. Uribe, Reactor Inspector
Approved By:
M. Haire, Chief
Project Branch A
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an Integrated Inspection at Comanche Peak Nuclear Power Plant in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and violations being considered in the NRCs assessment are summarized in the table below.
List of Findings and Violations
Failure to Incorporate Design Information Into System Test Procedures Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-02; 05000446/2018001-02 Closed None 71152 -
Problem Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI,
Test Control, for the licensees failure to ensure that station test procedures incorporated all requirements contained in applicable design documents. Specifically, the stations test procedures for the component cooling water system failed to test the safeguards loops supply and return train isolation valves for leakage. Excess leakage from these valves could prevent the performance of a safety function. This finding was entered into the licensees corrective action program as Condition Report CR-2017-012024.
Failure to Follow Commercial Grade Dedication Process Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-01; 05000446/2018001-01 Closed None 7111112 -
Maintenance Effectiveness The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to accomplish activities affecting quality in accordance with documented procedures.
Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms to safety related without following the requirements of station procedure ECE-6.02-03, Critical Characteristics Development. The licensee entered this issue into the corrective action program as Condition Reports CR-CR-2016-009733 and CR-2017-007811.
Failure to Provide an Adequate Procedure Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-03; 05000446/2018001-03 Closed None 71152 -
Problem Identification and Resolution The inspectors identified a Green, non-cited violation of Technical Specification 5.4.1,
Procedures, associated with the licensees failure to provide procedures appropriate to the circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C Equipment, did not contain adequate instructions for wiring current to pressure (I/P)converters for safety related components which resulted in the steam generator atmospheric relief valve I/P converters being placed in a seismically unqualified configuration. This finding was entered into the licensees corrective action program as Condition Report CR-2017-011922.
Inadequate Maintenance Procedure for Feedwater Valves Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-04; 05000446/2018001-04 Closed None 71153 -
Follow-up of Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed Green, non-cited violation of Technical Specification 5.4.1, Procedures, associated with the licensees failure to prescribe adequate procedures for performing maintenance on the feedwater bypass control valves. Specifically, the licensees procedure failed to specify the correct torque on the handwheel screw locknut, resulting in a loose locknut which led to a control valve failure and a turbine trip. This finding was entered into the licensees corrective action program as Condition Report CR-2017-009139.
Failure to Correct a Significant Condition Adverse to Quality Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-05; 05000446/2018001-05 Closed P.2 - Problem Identification and Resolution,
Evaluation 71153-Follow-up of Events and Notices of Enforcement Discretion The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, associated with the licensees failure to take corrective action for the identified cause of a significant condition adverse to quality. Specifically, a feedwater bypass control valve vibrated open resulting in a turbine trip and initiation of auxiliary feedwater. The licensee determined that the cause was an inadequate procedure for performing maintenance on the feedwater bypass control valves, but failed to correct the inadequate procedure after identifying it as the cause of a control valve failure and a turbine trip. This finding was entered into the licensees corrective action program as Condition Report CR-2018-000959.
Additional Tracking Items
Type Issue number Title Report Section Status LER 05000445;05000446/
2017-001-00; 05000445;05000446/
2017-001-01 Unanalyzed Condition Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies 71153 Closed LER 05000446/2017-001-00; 05000446/2017-001-01; 05000446/2017-001-02 Auxiliary Feedwater System Actuation During Unit 2 Turbine Trip 71153 Closed LER 05000446/2017-002-00 Manual Reactor Trip Due to Dropped Rods 71153 Closed LER 05000446/2017-003-00 Manual Reactor Trip due to trip of both Main Feedwater Pumps 71153 Closed VIO 05000445/2015008-01; 05000446/2015008-01 Failure to Evaluate the Lack of Missile Protection on the Turbine Driven Auxiliary Feedwater Pumps Steam Exhaust Piping 92702 Closed
PLANT STATUS
Unit 1 began the inspection period at approximately 100 percent power, and operated at full power for the rest of the inspection period.
Unit 2 began the inspection period at approximately 100 percent power, and operated at full power for the rest of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather (1 Sample)
The inspectors evaluated readiness for impending adverse weather conditions for severe thunderstorms on March 19, 2018.
71111.04 - Equipment Alignment
Partial Walkdown (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 emergency diesel generator 2-01 while diesel generator 2-02 was out of service in an unplanned maintenance outage, on February 9, 2018
- (2) Unit 2 Train B sequencer equipment during Train A actuation testing, on February 21, 2018
- (3) Unit 1 coolant charging pump 1-02 while coolant charging pump 1-01 was out of service for maintenance, on March 21, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the Unit 1 emergency diesel generators system on March 14, 2018.
===71111.05AQFire Protection Annual/Quarterly
Quarterly Inspection===
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Fire zone SG10a, Unit 1 emergency diesel generator A, on March 23, 2018
- (2) Fire zone SI12a, Unit 1 emergency diesel generator B, on March 23, 2018
- (3) Fire zone SH11, Unit 1 emergency diesel generator A day tank room, on March 23, 2018
- (4) Fire zone SJ13, Unit 1 emergency diesel generator B day tank room, on March 23, 2018
- (5) Fire zone EM63, Unit 2 cable spreading room, on March 26, 2018
71111.06Flood Protection Measures Internal Flooding
The inspectors evaluated internal flooding mitigation protections in the Unit 2 emergency diesel generator rooms on March 14, 2018.
71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification
The inspectors observed and evaluated a crew during a simulator evaluated scenario for licensed operator requalification training on February 27, 2018.
Operator Performance (1 Sample)
The inspectors observed and evaluated:
- (1) Unit 1 control room actions during testing of steam generator atmospheric relief valves, on March 6, 2018
- (2) Unit 1 control room operators response to the unexpected lifting of power operated relief valve 455A, on March 20, 2018
71111.12Maintenance Effectiveness Routine Maintenance Effectiveness
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
- (1) Unit 1 emergency diesel generators, on March 6, 2018
- (2) Unit 1 and Unit 2 steam generator atmospheric relief valves, on March 20, 2018
Quality Control (1 Sample)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:
- (1) Unit 1 and Unit 2 upgrade of series 200 diaphragm seals
71111.13Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 2 diesel generator 2-01 during unplanned maintenance on diesel 2-02, on January 11, 2018
- (2) Unit 1 train A service water/component cooling water outage, on January 23, 2018
- (3) Unit 2 component cooling water pump 2-02 recirculation flow control valve 2-HS-4537, on January 29, 2018
- (4) Unit 2 emergent maintenance on diesel generator 2-02 due to broken amphenol, on February 7, 2018
- (5) Unit 2 emergent maintenance on component cooling water pump 2-02 due to excessive shaft and bearing wear, on February 12, 2018
71111.15Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Unit 2, CR-2017-013643, 2-02 component cooling water heat exchange fouling, on January 8, 2018
- (2) Unit 1 and 2, CR-2017-010346, condensate storage tank level transmitter uncertainty, on January 10, 2018
- (3) Unit 1 and 2, IR-2018-000815, vent chiller X-04 liquid level too high, on January 30, 2018
- (4) Unit 2, CR-2018-000941, component cooling water pump 2-02 excessive shaft wear, on February 9, 2018
- (5) Unit 1, opening seismically qualified cabinet doors for maintenance, on February 15, 2018
- (6) Unit 1, CR-2018-001264, water in-leakage degrading concrete, on March 1, 2018
71111.18Plant Modifications
The inspectors evaluated the following temporary or permanent modifications:
- (1) Unit 2, component cooling water pump 2-02 increase in thrust bearing locknut torque due to identified degraded condition, on February 13, 2018
71111.19Post Maintenance Testing
The inspectors evaluated the following post maintenance tests:
- (1) Unit 2, diesel generator 2-02 following corrective maintenance, on January 16, 2018
- (2) Unit 2, diesel generator 2-02 following amphenol replacement, on February 9, 2018
- (3) Unit 2, component cooling water pump 2-02 following corrective maintenance, on February 12, 2018
- (4) Unit 2, centrifugal charging pump 2-01 following maintenance, on February 15, 2018
- (5) Unit 2, steam generator 2-03 atmospheric relief valve following wiring removal, on March 18, 2018
- (6) Unit 1, centrifugal charging pump 1-01 following maintenance, on March 28, 2018
===71111.22Surveillance Testing
The inspectors evaluated the following surveillance tests:
Routine===
- (1) Unit 1, OPT-214A diesel generator 1-02, on January 12, 2018
- (2) Unit 2, OPT-214B diesel generator 2-02, on March 12, 2018
- (3) Unit 2, OPT-214B diesel generator 2-01, on March 22, 2018
- (4) Unit 1, OPT-414A, blackout sequencer logic test, on March 29, 2018
In-service (2 Samples)
- (1) Unit 2, OPT-208B, component cooling water pump 2-02 recirculation flow control valve 2-HS-4537, on January 30, 2018
- (2) Unit 2, OPT-509, in-service testing of main steam isolation valves, on March 15, 2018
71114.06Drill Evaluation Emergency Planning Drill
The inspectors evaluated an extended loss of AC power to Unit 1 drill on February 14,
OTHER ACTIVITIES - BASELINE
71151Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below for the period from January 1 through December 31, 2017, for both Units 1 and 2:
- (1) IE01: Unplanned Scrams per 7000 Critical Hours Sample
- (2) IE03: Unplanned Power Changes per 7000 Critical Hours Sample
- (3) IE04: Unplanned Scrams with Complications (USwC) Sample
71152Problem Identification and Resolution Annual Follow-up of Selected Issues
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Unexpected lifting of steam generator atmospheric relief valves 1-PV-2327 and 2-PV-2327
- (2) Component cooling water supply cross connect valve leakage
71153Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
- (1) Licensee Event Report (LER) 05000445;05000446/2017-001-01, Unanalyzed Condition Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies, on January 11, 2017 [revisions 00 and 01 reviewed]
- (2) LER 05000446/2017-001-02, Auxiliary Feedwater System Actuation During Unit 2 Turbine Trip, on August 11, 2017 [revisions 00, 01, and 02 reviewed]
- (3) LER 05000446/2017-002-00, Manual Reactor Trip Due to Dropped Rods, on September 1, 2017
- (4) LER 05000446/2017-003-00, Manual Reactor Trip due to trip of both Main Feedwater Pumps, on November 25,
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
92702Followup on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution Confirmatory Orders
The inspectors reviewed the licensees response to NOV 05000445/2015008-01; 05000446/2015008-01 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance will be achieved for this violation is adequately addressed and captured on the docket.
INSPECTION RESULTS
Failure to Follow Commercial Grade Dedication Process Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-01; 05000446/2018001-01 Closed None
71111.12 - Maintenance
Effectiveness The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to accomplish activities affecting quality in accordance with documented procedures.
Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms to safety related without following the requirements of station procedure ECE-6.02-03, Critical Characteristics Development.
Description:
While reviewing information related to Licensee Event Report 05000445;05000446/2017-001-01, Unanalyzed Condition Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies, inspectors reviewed the licensees root cause analyses documented in Condition Report CR-2016-010346. During this review inspectors noted that the licensee had upgraded previously installed commercial grade material to safety related. Specifically, Ashcroft series 200 diaphragms were supplied to the licensee during initial construction as non-safety related parts and installed in the centrifugal coolant charging pumps and positive displacement pumps suction and discharge pressure indicators as such. Subsequently, in 2003 the licensee determined that the diaphragm seals were in fact part of the safety related pressure boundary and were required to be safety related, and the licensee upgraded the Ashcroft series 200 diaphragms to safety related components due to seismic boundary concerns.
However, the inspectors also noted that the licensees root cause analyses stated that the upgrade of the diaphragm seal assemblies did not appear to have resulted in any additional evaluation. Inspectors questioned this and asked for the licensees commercial grade dedication packages for the Ashcroft series 200 diaphragms. The licensee responded that they had not done a commercial grade dedication package because the diaphragms had been supplied as quality group C (safety related) by the vendor. Inspectors asked to see the vendor paperwork designating the components as quality group C but the licensee responded that they did not have copies of this paperwork and they would have to get it from the vendor.
During subsequent discussions with the vendor, the licensee determine that the Ashcroft series 200 diaphragms were in fact provided as quality group C but this designation did not mean they were safety related. In fact, the vendor specification sheet provided to the licensee designated quality group C as non-safety related commercial grade components.
Based on this, the licensee determined that they had made errors in their assumptions when upgrading the diaphragms in 2003. Specifically, the licensee had made errors in their interpretation of what the vendor quality group designator meant, and they did not have copies of the appropriate specifications/paperwork when upgrading the diaphragm seal assemblies. The licensee initiated Condition Report CR-2016-009733 to capture this issue in the stations corrective action program. Subsequently, the licensee determined that there were approximately 29 additional Ashcroft series 200 diaphragms that had been inappropriately upgraded to safety related without commercial grade dedication packages.
Inspectors determined that had the licensee followed the requirements of station procedure ECE-6.02-03, Critical Characteristics Development, when upgrading the Ashcroft series 200 diaphragms to safety related components this would have required them to review all applicable paperwork. As such, inspectors determined that the licensees failure to follow procedural requirement resulted in non-safety related components being installed in a safety related application.
Corrective Action(s): The licensee performed an operability determination that established a reasonable expectation of operability pending additional corrective actions which include commercial grade dedication of the affected diaphragm seals.
Corrective Action Reference(s): CR-2016-009733 and CR-2017-007811
Performance Assessment:
Performance Deficiency: The licensees failure to follow the requirements of procedure ECE-6.02-03 when upgrading the safety classification of material was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
Specifically, the use of unqualified materials could result in equipment not being available to function during design events such as response to a seismic event.
Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At-Power, Exhibit 4, External Events Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because the finding is a deficiency affecting the design or qualification of a mitigating system, structure, or component (SSC), but the SSC maintained its operability.
Cross-cutting Aspect: The inspectors determined that the performance deficiency occurred more than three years ago and was not indicative of current performance.
Enforcement:
Violation: Title 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings, of a type appropriate to the circumstances. Procedure ECE-6.02-03, Critical Characteristics Development, an Appendix B quality related procedure, provides instructions for the commercial grade dedication of materials and parts.
Contrary to the above, in 2003 when upgrading the safety classification of Ashcroft series 200 diaphragms to safety related, the licensee failed to accomplish activities affecting quality in accordance with documented instructions, procedures, or drawings, of a type appropriate to the circumstances. Specifically, the licensee failed to follow the requirements of procedure ECE-6.02-03 when upgrading the safety classification of material.
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Failure to Incorporate Design Information Into System Test Procedures Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-02; 05000446/2018001-02 Closed None
71152 - Problem
Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI, Test Control, for the licensees failure to ensure that station test procedures incorporated all requirements contained in applicable design documents. Specifically, the stations test procedures for the component cooling water system failed to test the safeguards loops supply and return train isolation valves for leakage. Excess leakage from these valves could prevent the performance of a safety function.
Description:
During fill and vent activities on the B train safeguards loop of the Unit 1 component cooling water system on October 24, 2017, the licensee noted a system pressure rise and determined the cause to be leakage past safeguards loops train A and B isolation valves 1-HV-4513 and 1-HV-4515 (respectively). The component cooling water system has four valves that close on an empty level in the surge tank to separate the safeguards loops from each other and from the non-safeguards loop. The licensee initiated Condition Report CR-2017-011897 to capture this issue in the stations corrective action program.
The inspectors reviewed this condition report and noted that the licensee had determined that the leakage past the valves was approximately 40.3 gallons per minute (gpm). Inspectors noted that this exceeded the allowable leakage limit of 37 gpm and the licensee had performed an operability determination and determined that the valves were operable but degraded based on an engineering evaluation. During their review of the operability evaluation, the inspectors noted the following:
- Makeup to the surge tank is normally an automatic function; however, during events that result in a loss of instrument air, automatic makeup to the surge tank is lost and manual makeup is required but not assumed to start for 30 minutes following receipt of the empty alarm.
- When the surge tank reaches the empty level setpoint, this causes safeguards loops supply and return train isolation valves 1-HV-4512, 1-HV-4514, 1-HV-4513, and 1-HV-4515 to close which separates the safeguards loops from each other and isolates them from the non-safeguards loop fast enough to prevent loss of inventory from at least one of the safeguards loops.
- The surge tank design analysis assumes a system leak rate of 1 gpm (0.4 gpm for Unit 2).
- Safeguards loop supply and return isolation valve design stroke time is 45 seconds.
- Worst case break is in the non-seismic piping in the non-safeguards loop (seismic event will result in a loss of offsite power which stops automatic makeup to the surge tank).
- Therefore, based on the operator response time and system leak rate the allowable train leakage limit is 37 gpm [10 gpm for Unit 2]. This ensures that there is adequate volume in the surge tank below the empty level to accommodate the water depletion due to postulated line break in the non-safeguard loop or the opposite train during the closing time of the isolation valves, without depleting the tank volume.
- The licensee used measured stroke time of the valves, 27 seconds for both valves, as the assumed closing time and determined that the allowed train leakage was 46 gpm.
Inspectors also noted that previously the licensee had experienced a similar issue.
Specifically, on May 15, 2016, during train A restoration activities, the licensee identified that train A and B isolation valves 1-HV-4512 and 1-HV-4514 (respectively) were leaking by at approximately 43.55 gpm.
Inspectors questioned how the licensee was monitoring the system for leakage and queried the licensee about what testing is done on the system. The licensee responded that walk downs were done looking for leakage. Inspectors asked if the licensee performed train leakage test since the supply and return isolation valves were potential leak paths that could not be identified by walk down. The licensee responded that no testing looking for leaks was conducted, nor did the licensee believe they were required to do so.
However, following a review of the stations Updated Final Safety Analysis Report, Chapters 3 and 9, the inspectors determined that:
- The component cooling water system and its safeguards loop components are required to withstand the effects of natural phenomena, such as seismic events, without loss of capability to perform its safety function [remove heat from safeguards loop components]. Therefore, one of the safeguards loops of the component cooling water system is required to remain operational during and following a failure of a non-seismic component in the non-safeguards loop following a seismic event assuming a single failure in the other loop [makes that loop unavailable].
- The closure time of the safeguards loop isolation valves and the train leakage limit are design requirements since they affect the ability of the system to perform its safety function.
Further, Title 10 CFR 50, Appendix B, Criterion XI requires, in part, that a test program shall be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in service is identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents.
Based on this, inspectors determined that the licensees practice of walking down the component cooling water system looking for leakage was not adequate and that the licensee should be testing the safeguards loops for leakage since leakage past the loop isolation valves could prevent the system from performing its safety function. Inspectors determined that this was applicable to both units.
Inspectors determined that this issue did not represent current performance because the licensee had not reviewed nor revised the testing methodology for the system in the last three years.
Corrective Action(s): The licensee performed an operability determination that established a reasonable expectation of operability pending development of additional corrective actions.
Corrective Action Reference(s): Condition Report CR-2017-012024
Performance Assessment:
Performance Deficiency: The licensees failure to incorporate design information into system test procedures was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, not monitoring for system leakage could result in a leak rate that would prevent the performance of system safety function.
Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At Power, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because:
- (1) it was not a design deficiency;
- (2) it did not represent a loss of system and/or function;
- (3) it did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
- (4) it did not result in the loss of a high safety significant nontechnical specification train.
Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the performance deficiency was not reflective of current performance.
Enforcement:
Violation: Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that a test program shall be established to assure that all testing required to demonstrate components will perform satisfactorily in service is identified and performed in accordance with written procedures which incorporate the requirements and acceptance limits contained in applicable design documents.
Contrary to the above, from initial construction until present, the licensee failed to established a test program to assure that all testing required to demonstrate components will perform satisfactorily in service is identified and performed in accordance with written procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Specifically, the licensee failed to incorporate design information into system test procedures for the component cooling water system relative to leak testing for the safeguards loops supply and return train isolation valves.
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Failure to Provide Adequate Procedure Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018001-03; 05000446/2018001-03 Closed None
71152 - Problem
Identification and Resolution The inspectors identified a Green, non-cited violation of Technical Specification (TS) 5.4.1, Procedures, associated with the licensees failure to provide procedures appropriate to the circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C Equipment, did not contain adequate instructions for wiring current-to-pressure (I/P)converters for safety related components which resulted in the steam generator atmospheric relief valve I/P converters being placed in a seismically unqualified configuration.
Description:
On October 24, 2017, it was reported to the control room that steam generator 2-03 atmospheric dump valve 2-PV-2327 was leaking. The valve was found to be open approximately 20 percent. This issue was entered into the corrective action program as Condition Report CR-2017-011922. During the licensees investigation they noted that work had been going on in the vicinity of the I/P converter for valve 2-PV-2327 and that maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold pole. The licensee also found that the I/P converter output settings were high. When the licensee removed the cover of the converter they discovered that excess lead wires stored in the housing were in contact with moveable parts of the converter which caused valve 2-PV-2327 to open. The licensee moved the lead wires so they were no longer in contact with the moveable parts of the I/P converter.
Subsequently, on October 30, 2017, operators noted that steam generator 1-03 atmospheric dump valve 1-PV-2327 was not indicating fully shut as demanded. The valve was found to be open approximately 20 percent. This issue was entered into the corrective action program as Condition Report CR-2017-012141. During the licensees investigation they noted that work had been going on in the vicinity of the I/P converter for valve 1-PV-2327 and that maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold pole. The licensee also found that the I/P converter output settings were high. When the licensee removed the cover of the converter they discovered that excess lead wires stored in the housing were in contact with moveable parts of the converter which caused valve 1-PV-2327 to open. The licensee moved the lead wires so they were no longer in contact with the moveable parts of the I/P converter.
The licensee performed an equipment cause analysis checklist and determined that inadequate work practices was the cause of the issues. Inspectors questioned the licensees identified cause in that that both issues appeared to happen after the housing for the converters was struck with a scaffold pole, and raised concerns regarding seismic qualification of the converters.
These concerns were expressed to the licensee who subsequently determined that the excess wiring in the converter housing was not in a qualified seismic configuration. The licensee determined that this configuration had existed most likely since initial installation of the I/P converters and this was due to inadequate guidance provided in station procedure INC-2085, Rework and Replacement of I&C Equipment, for maintenance personnel regarding proper storage of excess field leads. Specifically, the procedure did not provide sufficient guidance to ensure that electrical lead wire or other components within the I/P converter were sufficiently secured to preclude contact with the moveable parts of the I/P converter, in order to ensure the function and seismic qualification of the components were maintained.
Corrective Action(s): The licensee performed an operability determination that established a reasonable expectation of operability, developed work orders to remove the excess wiring from the converters, and changed procedure INC-2085 to not allow excess wiring in the converter housing.
Corrective Action Reference(s): Condition Report CR-2017-011922
Performance Assessment:
Performance Deficiency: The licensees failure to prescribe adequate procedures to perform quality related activities associated with the steam generator atmospheric relief valve I/P converters was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the improper training of the lead wires resulted in the I/P converters being in a non-seismically qualified configuration.
Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding was of very low safety significance (Green)because:
- (1) it was not a design deficiency;
- (2) it did not represent a loss of system and/or function;
- (3) it did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
- (4) it did not result in the loss of a high safety significant non-technical specification train.
Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the performance deficiency was not reflective of current performance.
Enforcement:
Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-related equipment be performed in accordance with written procedures appropriate to the circumstances.
Contrary to the above, from initial installation through March 13, 2018, for maintenance activities on steam generator atmospheric relief valve I/P converters, an activity that can affect the performance of safety-related equipment to which Technical Specification 5.4.1.a applies, the licensee failed to assure that the maintenance procedures were appropriate to the circumstances.
Disposition: This violation is being treated as a Non-Cited Violation, consistent with Section 2.3.2 of the Enforcement Policy.
Inadequate Maintenance Procedure for Feedwater Valves Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-04; 05000446/2018001-04 Closed None 71153 - Follow-up of Events and Notices of Enforcement Discretion The inspectors reviewed a self-revealed, Green non-cited violation of TS 5.4.1, Procedures, associated with the licensees failure to prescribe adequate procedures for performing maintenance on the feedwater bypass control valves. Specifically, the licensees procedure failed to specify the correct torque on the hand wheel screw locknut, resulting in a loose locknut which led to a control valve failure and a turbine trip.
Description:
During the Unit 2 startup on August 11, 2017, following a forced outage, a turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main generator on the grid. The turbine trip and initiation of auxiliary feedwater was caused by steam generator 2-02 water level rising above the high level setpoint due to a failure of the steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand. These valves are equipped with a valve hand wheel locknut designed to prevent the manual hand wheel from rotating due to vibration. The valve failed to close because the valve hand wheel locknut had backed off its normal fully closed position allowing the manual hand wheel to rotate open and preventing the valve from closing. The licensee performed a review of work history on the valve and identified work activities during which the locknut was manipulated.
The licensee determined that the locknut was last manipulated during replacement of the 2-LV-2163 elastomers on October 15, 2015. The work was done in accordance with MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, Section 8.5. The guidance in MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN hand wheel screw locknut, but does not include specific acceptance criteria or guidance on the required torque to apply when tightening. For comparison, MSM-C0-6602 section 8.4 also includes a step to tighten the locknut, but states TIGHTEN hand wheel screw locknut snug tight. The phrase snug tight is used by licensee maintenance personnel to denote a qualitative torque value to apply to a component to ensure it will not come loose during normal operation. The licensee determined that the locknut needed to be left snug tight, and that the guidance in section 8.5 was not adequate. The inspectors determined that the inadequate procedural guidance had existed in the procedure since October 2007.
Inspectors determined that the failure of steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand was a significant condition adverse to quality because this issue resulted in a turbine trip and initiation of auxiliary feedwater, and could have resulted in a reactor scram
Corrective Action(s): The licensee verified all feedwater bypass control valve locknuts have been properly tightened in accordance with the appropriate qualitative torque value of snug tight.
Corrective Action Reference(s): CR-2017-009139
Performance Assessment:
Performance Deficiency: The licensees failure to prescribe adequate procedures to perform quality related activities associated with the feedwater bypass control valves was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the inadequate procedure resulted in a failure of a feedwater bypass control valve leading to an unplanned turbine trip and initiation of auxiliary feedwater.
Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition.
Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the performance deficiency was not reflective of current performance.
Enforcement:
Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-related equipment be performed in accordance with written procedures appropriate to the circumstances.
Contrary to the above, from October 2007 through August 2017, for maintenance activities on the feedwater bypass control valves, an activity that can affect the performance of safety-related equipment to which Technical Specification 5.4.1.a applies, the licensee failed to assure that the maintenance procedures were appropriate to the circumstances.
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Failure to Correct a Significant Condition Adverse to Quality Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000445/2018001-05; 05000446/2018001-05 Closed P.2 - Problem Identification and Resolution, Evaluation 71153 - Follow-up of Events and Notices of Enforcement Discretion The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, associated with the licensees failure to take corrective action to preclude repetition of a significant condition adverse to quality. Specifically, a feedwater bypass control valve vibrated open resulting in a turbine trip and initiation of auxiliary feedwater. The licensee determined that the cause was an inadequate procedure for performing maintenance on the feedwater bypass control valves, but failed to correct the inadequate procedure after identifying it as the cause of a control valve failure and a turbine trip.
Description:
During the Unit 2 startup on August 11, 2017, following a forced outage, a turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main generator on the grid (refer to NCV 05000445/2018001-04; 05000446/2018001-04 above).
The turbine trip and initiation of auxiliary feedwater was caused by steam generator 2-02 water level rising above the high level setpoint due to a failure of the steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand. Inspectors determined that this was a significant condition adverse to quality because this issue resulted in a turbine trip and initiation of auxiliary feedwater, and could have resulted in a reactor scram.
The licensee determined that the valve failed to close because the valve hand wheel locknut had backed off its normal fully closed position, preventing the valve from closing. The licensee performed a cause evaluation and identified that MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, contained inadequate guidance for restoration of the valve following maintenance. The guidance in MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN hand wheel screw locknut, but does not include specific acceptance criteria or guidance on the required torque to apply when tightening. Section 8.5 is used to perform elastomer replacement on these valves and was last used on 2-LV-2163 during replacement of the elastomers on October 15, 2015. Although the procedure contained inadequate guidance in section 8.5, the procedure also contains a section for general reassembly of the valve. MSM-C0-6602 section 8.4 includes a step to tighten the locknut, but states TIGHTEN hand wheel screw locknut snug tight. The phrase snug tight is used by licensee maintenance personnel to denote a qualitative torque value to apply to a component to ensure it will not come loose during normal operation. The licensee, in developing their corrective action plan, conflated section 8.4 and 8.5 and erroneously credited the correct step in section 8.4 as a corrective action for the inadequate step in section 8.5. The licensee assumed the corrective action had been completed during a procedural revision in 2012, and closed the corrective action plan without correcting section 8.5.
The inspectors reviewed the cause evaluation and corrective actions and identified that the licensee had failed to correct the inadequate procedure. The inspectors determined that MSM-C0-6602 section 8.5, step 8.5.43 was not revised, and no action was planned to revise it. The inspectors determined this to be a result of the licensees cause evaluation failing to identify the specific inadequate procedural step that caused the failure and as a result did not correct the deficiency.
The inspectors determined that the licensee had failed to implement corrective actions to preclude repetition of a significant condition adverse to quality.
Corrective Action(s): The licensee has verified all feedwater bypass control valve locknuts have been properly tightened, and changed procedure MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, step 8.5.43 to require the locknut to be tightened snug tight.
Corrective Action Reference(s): CR-2018-000959
Performance Assessment:
Performance Deficiency: The licensees failure to implement corrective actions to preclude repetition of a significant condition adverse to quality was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it adversely affected the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the inadequate procedure could reasonably be expected to result in another failure of the control valve and subsequent turbine trip.
Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events Screening Questions, the inspectors determined the finding was of very low safety significance (Green) because it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition.
Cross-cutting Aspect: The finding was assigned a cross-cutting aspect of evaluation because the licensee did not thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. (P.2)
Enforcement:
Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that, for significant conditions adverse to quality, measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition.
Contrary to the above, from August 2017 through February 2018, the licensee failed to establish measures to assure corrective action was taken to preclude repetition of a significant condition adverse to quality. Specifically, the licensee failed to correct the cause of the event by correcting the inadequate maintenance procedure for the feedwater bypass control valves.
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
The inspectors confirmed that proprietary information was controlled to protect from public disclosure.
On March 31, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. T. McCool, Site Vice President, and other members of the licensee staff.
THIRD PARTY REVIEWS
Inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the inspection period.
DOCUMENTS REVIEWED
7111112 - Maintenance Effectiveness
Condition Reports
CR-2016-009733
CR-2017-007811
CR-2016-010346
CR-2016-008375
CR-2003-000664
Procedures
(Number)
Title
Revision
Or Date
ECE-6.02-03
Critical Characteristics Development
5b
71152 - Problem Identification and Resolution
Condition Reports
CR-2017-012024
CR-2017-011897
CR-2016-004715
CR-2017-011922
CR-2017-012141
CR-2017-012144
CR-2018-000909
CR-2017-011944
CR-2018-002058
CR-2018-001629
Work Orders
3793710
3505655
3793738
3-01-330488-02
3-01-330490-02
3-01-332709-01
3-01-330492-02
4793333
5516071
5435660
20265
20201
25302
20253
Procedures
(Number)
Title
Revision
Or Date
MSM-C0-8837
Fisher Butterfly Valve Rework
ICA-101
I&C Work Control
INC-2085
Rework and Replacement of I&C Equipment
INC-4270A
Channel Calibration Power Relief Valve Control
Steam Generator 3 Channel 2327
Miscellaneous Documents
Number
Title
Revision
or Date
ME(B)-073
CCW Surge Tank Volume
SEQSP-MS-78-01
Fisher Air Operated Globe Valve Model 8X6 EWP
71153 - Follow-up of Events and Notices of Enforcement Discretion
Condition Reports
CR-2017-009139
CR-2018-000959
CR-2013-006702
CR-2017-005448
Procedures
(Number)
Title
Revision
Or Date
MSM-C0-6602
Fisher Diaphragm Actuator Maintenance
K. Peters
COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT
05000445/2018001 AND 05000446/2018001 - DATED MAY 8, 2018
DISTRIBUTION
KKennedy, RA
SMorris, DRA
AVegel, DRP
MShaffer, DRS
JClark, DRS
RLantz, DRP
JJosey, DRP
RKumana, DRP
MHaire, DRP
RAlexander, DRP
LNewman, DRP
IAnchondo, DRS
DLackey, DRP
JBowen, RIV/OEDO
SKirkwood, RC
VDricks, ORA
JWeil, OCA
MOBanion, NRR
AMoreno, RIV/OCA
BMaier, RSLO
GGeorge, IPAT
EUribe, IPAT
MHerrera, DRMA
RIV ACES
ROP Reports
Electronic Distribution for Comanche Peak Nuclear Power Plant
OFFICIAL RECORD COPY
ADAMS ACCESSION NUMBER: ML18127A572
SUNSI Review
By: MSH/rdr
Yes No
Non-Sensitive
Sensitive
Publicly Available Keyword:
Non-Publicly Available NRC-002
OFFICE
SRI:DRP/A
RI:DRP/A
SPE:DRP/A
BC:EB1
BC:EB2
BC:OB
NAME
JJosey
RKumana
RAlexander
TFarnholtz
JDrake
VGaddy
SIGNATURE
/RA/
/RA/
/RA/
/RA/
/RA/
/RA/
DATE
04/30/18
04/30/18
04/27/18
04/26/18
04/26/18
04/26/18
OFFICE
RI:DRP/A
RI:DRP/A
BC:PSB2
TL-IPAT
BC:DRP/A
NAME
IAnchondo
EUribe
HGepford
GGeorge
MHaire
SIGNATURE
/RA/
/RA/
/RA/
/RA/
/RA/
DATE
04/26/2018
05/01/18
05/01/18
04/27/18
05/8/2018
May 8, 2018
Mr. Ken
- J. Peters, Senior Vice President
and Chief Nuclear Officer
Vistra Operations Company LLC
P.O. Box 1002
Glen Rose, TX 76043
SUBJECT:
COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED
INSPECTION REPORT 05000445/2018001 AND 05000446/2018001
Dear Mr. Peters:
On March 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 5, 2018, the NRC
inspectors discussed the results of this inspection with Mr. Tom McCool, Site Vice President,
and other members of your staff. The results of this inspection are documented in the enclosed
report.
NRC inspectors documented five findings of very low safety significance (Green) in this report.
All of these findings involved violations of NRC requirements. The NRC is treating these
violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement
Policy.
If you contest the violations or significance of these NCVs, you should provide a response within
days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with
copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the
NRC resident inspector at the Comanche Peak Nuclear Power Plant.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the
- U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the
NRC resident inspector at the Comanche Peak Nuclear Power Plant.
K. Peters
This letter, its enclosure, and your response (if any) will be made available for public inspection
and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document
Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for
Withholding.
Sincerely,
/RA/
Mark
- S. Haire, Chief
Project Branch A
Division of Reactor Projects
Docket Nos. 5000445 and 5000446
License Nos. NPF-87 and NPF-89
Enclosure:
Inspection Report 05000445/2017004
and 05000446/2017004
w/ Attachment:
Documents Reviewed
U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Docket Numbers:
05000445, 05000446
License Numbers:
Report Numbers:
05000445/2018001 and 05000446/2018001
Enterprise Identifier: I-2018-001-0011
Licensee:
Vistra Operations Company, LLC
Facility:
Comanche Peak Nuclear Power Plant, Units 1 and 2
Location:
Glen Rose, Texas
Inspection Dates:
January 1, 2018 to March 31, 2018.
Inspectors:
- J. Josey, Senior Resident Inspector
- R. Kumana, Resident Inspector
- I. Anchondo, Reactor Inspector
- E. Uribe, Reactor Inspector
Approved By:
- M. Haire, Chief
Project Branch A
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting an Integrated Inspection at Comanche Peak Nuclear Power Plant in
accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs
program for overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and
violations being considered in the NRCs assessment are summarized in the table below.
List of Findings and Violations
Failure to Incorporate Design Information Into System Test Procedures
Cornerstone Significance
Cross-cutting
Aspect
Report
Section
Mitigating
Systems
Green
Closed
None
71152 -
Problem
Identification
and
Resolution
The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI,
Test Control, for the licensees failure to ensure that station test procedures incorporated all
requirements contained in applicable design documents. Specifically, the stations test
procedures for the component cooling water system failed to test the safeguards loops supply
and return train isolation valves for leakage. Excess leakage from these valves could prevent
the performance of a safety function. This finding was entered into the licensees corrective
action program as Condition Report CR-2017-012024.
Failure to Follow Commercial Grade Dedication Process
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Mitigating
Systems
Green
Closed
None
7111112 -
Maintenance
Effectiveness
The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to
accomplish activities affecting quality in accordance with documented procedures.
Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms
to safety related without following the requirements of station procedure ECE-6.02-03, Critical
Characteristics Development. The licensee entered this issue into the corrective action
program as Condition Reports CR-CR-2016-009733 and CR-2017-007811.
Failure to Provide an Adequate Procedure
Cornerstone Significance
Cross-cutting
Aspect
Report
Section
Mitigating
Systems
Green
Closed
None
71152 -
Problem
Identification
and
Resolution
The inspectors identified a Green, non-cited violation of Technical Specification 5.4.1,
Procedures, associated with the licensees failure to provide procedures appropriate to the
circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C
Equipment, did not contain adequate instructions for wiring current to pressure (I/P)
converters for safety related components which resulted in the steam generator atmospheric
relief valve I/P converters being placed in a seismically unqualified configuration. This finding
was entered into the licensees corrective action program as Condition Report CR-2017-
011922.
Inadequate Maintenance Procedure for Feedwater Valves
Cornerstone Significance
Cross-cutting
Aspect
Report
Section
Initiating
Events
Green
Closed
None
71153 -
Follow-up of
Events and
Notices of
Enforcement
Discretion
The inspectors reviewed a self-revealed Green, non-cited violation of Technical Specification 5.4.1, Procedures, associated with the licensees failure to prescribe adequate
procedures for performing maintenance on the feedwater bypass control valves. Specifically,
the licensees procedure failed to specify the correct torque on the handwheel screw locknut,
resulting in a loose locknut which led to a control valve failure and a turbine trip. This finding
was entered into the licensees corrective action program as Condition Report CR-2017-
009139.
Failure to Correct a Significant Condition Adverse to Quality
Cornerstone Significance
Cross-cutting
Aspect
Report
Section
Initiating
Events
Green
Closed
P.2 - Problem
Identification
and
Resolution,
Evaluation
71153-
Follow-up of
Events and
Notices of
Enforcement
Discretion
The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, associated with the licensees failure to take corrective action for the
identified cause of a significant condition adverse to quality. Specifically, a feedwater bypass
control valve vibrated open resulting in a turbine trip and initiation of auxiliary feedwater. The
licensee determined that the cause was an inadequate procedure for performing maintenance
on the feedwater bypass control valves, but failed to correct the inadequate procedure after
identifying it as the cause of a control valve failure and a turbine trip. This finding was entered
into the licensees corrective action program as Condition Report CR-2018-000959.
Additional Tracking Items
Type
Issue number
Title
Report
Section
Status
LER
05000445;05000446/
2017-001-00;
05000445;05000446/
2017-001-01
Unanalyzed Condition Involving
Teflon Installed in Containment
Spray Pump Diaphragm Seal
Assemblies
Closed
05000446/2017-001-01;
05000446/2017-001-02
Auxiliary Feedwater System
Actuation During Unit 2 Turbine
Trip
Closed
Manual Reactor Trip Due to
Dropped Rods
Closed
Manual Reactor Trip due to trip
of both Main Feedwater Pumps
Closed
Failure to Evaluate the Lack of
Missile Protection on the
Turbine Driven Auxiliary
Feedwater Pumps Steam
Exhaust Piping
2702
Closed
PLANT STATUS
Unit 1 began the inspection period at approximately 100 percent power, and operated at full
power for the rest of the inspection period.
Unit 2 began the inspection period at approximately 100 percent power, and operated at full
power for the rest of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem
Identification and Resolution. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather (1 Sample)
The inspectors evaluated readiness for impending adverse weather conditions for severe
thunderstorms on March 19, 2018.
71111.04 - Equipment Alignment
Partial Walkdown (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1) Unit 2 emergency diesel generator 2-01 while diesel generator 2-02 was out of service in
an unplanned maintenance outage, on February 9, 2018
(2) Unit 2 Train B sequencer equipment during Train A actuation testing, on
February 21, 2018
(3) Unit 1 coolant charging pump 1-02 while coolant charging pump 1-01 was out of service
for maintenance, on March 21, 2018
Complete Walkdown (1 Sample)
The inspectors evaluated system configurations during a complete walkdown of the
Unit 1 emergency diesel generators system on March 14, 2018.
71111.05AQFire Protection Annual/Quarterly
Quarterly Inspection (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected
areas:
(1) Fire zone SG10a, Unit 1 emergency diesel generator A, on March 23, 2018
(2) Fire zone SI12a, Unit 1 emergency diesel generator B, on March 23, 2018
(3) Fire zone SH11, Unit 1 emergency diesel generator A day tank room, on March 23, 2018
(4) Fire zone SJ13, Unit 1 emergency diesel generator B day tank room, on March 23, 2018
(5) Fire zone EM63, Unit 2 cable spreading room, on March 26, 2018
71111.06Flood Protection Measures
Internal Flooding (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the Unit 2 emergency
diesel generator rooms on March 14, 2018.
71111.11Licensed Operator Requalification Program and Licensed Operator Performance
Operator Requalification (1 Sample)
The inspectors observed and evaluated a crew during a simulator evaluated scenario for
licensed operator requalification training on February 27, 2018.
Operator Performance (1 Sample)
The inspectors observed and evaluated:
(1) Unit 1 control room actions during testing of steam generator atmospheric relief valves,
on March 6, 2018
(2) Unit 1 control room operators response to the unexpected lifting of power operated relief
valve 455A, on March 20, 2018
71111.12Maintenance Effectiveness
Routine Maintenance Effectiveness (2 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated
with the following equipment and/or safety significant functions:
(1) Unit 1 emergency diesel generators, on March 6, 2018
(2) Unit 1 and Unit 2 steam generator atmospheric relief valves, on March 20, 2018
Quality Control (1 Sample)
The inspectors evaluated maintenance and quality control activities associated with the
following equipment performance issues:
(1) Unit 1 and Unit 2 upgrade of series 200 diaphragm seals
71111.13Maintenance Risk Assessments and Emergent Work Control (5 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent
work activities:
(1) Unit 2 diesel generator 2-01 during unplanned maintenance on diesel 2-02, on
January 11, 2018
(2) Unit 1 train A service water/component cooling water outage, on January 23, 2018
(3) Unit 2 component cooling water pump 2-02 recirculation flow control valve 2-HS-4537,
on January 29, 2018
(4) Unit 2 emergent maintenance on diesel generator 2-02 due to broken amphenol, on
February 7, 2018
(5) Unit 2 emergent maintenance on component cooling water pump 2-02 due to excessive
shaft and bearing wear, on February 12, 2018
71111.15Operability Determinations and Functionality Assessments (6 Samples)
The inspectors evaluated the following operability determinations and functionality
assessments:
(1) Unit 2, CR-2017-013643, 2-02 component cooling water heat exchange fouling, on
January 8, 2018
(2) Unit 1 and 2, CR-2017-010346, condensate storage tank level transmitter uncertainty,
on January 10, 2018
(3) Unit 1 and 2, IR-2018-000815, vent chiller X-04 liquid level too high, on
January 30, 2018
(4) Unit 2, CR-2018-000941, component cooling water pump 2-02 excessive shaft wear, on
February 9, 2018
(5) Unit 1, opening seismically qualified cabinet doors for maintenance, on
February 15, 2018
(6) Unit 1, CR-2018-001264, water in-leakage degrading concrete, on March 1, 2018
71111.18Plant Modifications (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
(1) Unit 2, component cooling water pump 2-02 increase in thrust bearing locknut torque
due to identified degraded condition, on February 13, 2018
71111.19Post Maintenance Testing (6 Samples)
The inspectors evaluated the following post maintenance tests:
(1) Unit 2, diesel generator 2-02 following corrective maintenance, on January 16, 2018
(2) Unit 2, diesel generator 2-02 following amphenol replacement, on February 9, 2018
(3) Unit 2, component cooling water pump 2-02 following corrective maintenance, on
February 12, 2018
(4) Unit 2, centrifugal charging pump 2-01 following maintenance, on February 15, 2018
(5) Unit 2, steam generator 2-03 atmospheric relief valve following wiring removal, on
March 18, 2018
(6) Unit 1, centrifugal charging pump 1-01 following maintenance, on March 28, 2018
71111.22Surveillance Testing
The inspectors evaluated the following surveillance tests:
Routine (4 Samples)
(1) Unit 1, OPT-214A diesel generator 1-02, on January 12, 2018
(2) Unit 2, OPT-214B diesel generator 2-02, on March 12, 2018
(3) Unit 2, OPT-214B diesel generator 2-01, on March 22, 2018
(4) Unit 1, OPT-414A, blackout sequencer logic test, on March 29, 2018
In-service (2 Samples)
(1) Unit 2, OPT-208B, component cooling water pump 2-02 recirculation flow control
valve 2-HS-4537, on January 30, 2018
(2) Unit 2, OPT-509, in-service testing of main steam isolation valves, on March 15, 2018
71114.06Drill Evaluation
Emergency Planning Drill (1 Sample)
The inspectors evaluated an extended loss of AC power to Unit 1 drill on
February 14, 2018.
OTHER ACTIVITIES - BASELINE
71151Performance Indicator Verification (6 Samples)
The inspectors verified licensee performance indicators submittals listed below for the
period from January 1 through December 31, 2017, for both Units 1 and 2:
(1)
IE01: Unplanned Scrams per 7000 Critical Hours Sample
(2)
IE03: Unplanned Power Changes per 7000 Critical Hours Sample
(3)
IE04: Unplanned Scrams with Complications (USwC) Sample
71152Problem Identification and Resolution
Annual Follow-up of Selected Issues (2 Samples)
The inspectors reviewed the licensees implementation of its corrective action program
related to the following issues:
(1) Unexpected lifting of steam generator atmospheric relief valves 1-PV-2327
and 2-PV-2327
(2) Component cooling water supply cross connect valve leakage
71153Follow-up of Events and Notices of Enforcement Discretion
Licensee Event Reports (4 Samples)
The inspectors evaluated the following licensee event reports which can be accessed at
https://lersearch.inl.gov/LERSearchCriteria.aspx:
(1) Licensee Event Report (LER) 05000445;05000446/2017-001-01, Unanalyzed Condition
Involving Teflon Installed in Containment Spray Pump Diaphragm Seal Assemblies, on
January 11, 2017 [revisions 00 and 01 reviewed]
(2) LER 05000446/2017-001-02, Auxiliary Feedwater System Actuation During Unit 2
Turbine Trip, on August 11, 2017 [revisions 00, 01, and 02 reviewed]
(3) LER 05000446/2017-002-00, Manual Reactor Trip Due to Dropped Rods, on
September 1, 2017
(4) LER 05000446/2017-003-00, Manual Reactor Trip due to trip of both Main Feedwater
Pumps, on November 25, 2017
OTHER ACTIVITIES - TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
2702Followup on Traditional Enforcement Actions Including Violations, Deviations,
Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution
Confirmatory Orders
The inspectors reviewed the licensees response to NOV 05000445/2015008-01;
05000446/2015008-01 and determined that the reason, corrective actions taken and
planned to address recurrence, and the date when full compliance will be achieved for this
violation is adequately addressed and captured on the docket.
INSPECTION RESULTS
Failure to Follow Commercial Grade Dedication Process
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Mitigating
Systems
Green
Closed
None
71111.12 -
Maintenance
Effectiveness
The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to
accomplish activities affecting quality in accordance with documented procedures.
Specifically, the licensee upgraded the safety classification of Ashcroft series 200 diaphragms
to safety related without following the requirements of station procedure ECE-6.02-03,
Critical Characteristics Development.
Description: While reviewing information related to Licensee Event Report
05000445;05000446/2017-001-01, Unanalyzed Condition Involving Teflon Installed in
Containment Spray Pump Diaphragm Seal Assemblies, inspectors reviewed the licensees
root cause analyses documented in Condition Report CR-2016-010346. During this review
inspectors noted that the licensee had upgraded previously installed commercial grade
material to safety related. Specifically, Ashcroft series 200 diaphragms were supplied to the
licensee during initial construction as non-safety related parts and installed in the centrifugal
coolant charging pumps and positive displacement pumps suction and discharge pressure
indicators as such. Subsequently, in 2003 the licensee determined that the diaphragm seals
were in fact part of the safety related pressure boundary and were required to be safety
related, and the licensee upgraded the Ashcroft series 200 diaphragms to safety related
components due to seismic boundary concerns.
However, the inspectors also noted that the licensees root cause analyses stated that the
upgrade of the diaphragm seal assemblies did not appear to have resulted in any additional
evaluation. Inspectors questioned this and asked for the licensees commercial grade
dedication packages for the Ashcroft series 200 diaphragms. The licensee responded that
they had not done a commercial grade dedication package because the diaphragms had
been supplied as quality group C (safety related) by the vendor. Inspectors asked to see the
vendor paperwork designating the components as quality group C but the licensee responded
that they did not have copies of this paperwork and they would have to get it from the vendor.
During subsequent discussions with the vendor, the licensee determine that the Ashcroft
series 200 diaphragms were in fact provided as quality group C but this designation did not
mean they were safety related. In fact, the vendor specification sheet provided to the
licensee designated quality group C as non-safety related commercial grade components.
Based on this, the licensee determined that they had made errors in their assumptions when
upgrading the diaphragms in 2003. Specifically, the licensee had made errors in their
interpretation of what the vendor quality group designator meant, and they did not have
copies of the appropriate specifications/paperwork when upgrading the diaphragm seal
assemblies. The licensee initiated Condition Report CR-2016-009733 to capture this issue in
the stations corrective action program. Subsequently, the licensee determined that there
were approximately 29 additional Ashcroft series 200 diaphragms that had been
inappropriately upgraded to safety related without commercial grade dedication packages.
Inspectors determined that had the licensee followed the requirements of station procedure
ECE-6.02-03, Critical Characteristics Development, when upgrading the Ashcroft series 200
diaphragms to safety related components this would have required them to review all
applicable paperwork. As such, inspectors determined that the licensees failure to follow
procedural requirement resulted in non-safety related components being installed in a safety
related application.
Corrective Action(s): The licensee performed an operability determination that established a
reasonable expectation of operability pending additional corrective actions which include
commercial grade dedication of the affected diaphragm seals.
Corrective Action Reference(s): CR-2016-009733 and CR-2017-007811
Performance Assessment:
Performance Deficiency: The licensees failure to follow the requirements of procedure
ECE-6.02-03 when upgrading the safety classification of material was a performance
deficiency.
Screening: The inspectors determined the performance deficiency was more than minor
because it adversely affected the equipment performance attribute of the Mitigating Systems
Cornerstone and affected the cornerstone objective to ensure availability, reliability, and
capability of systems that respond to initiating events to prevent undesirable consequences.
Specifically, the use of unqualified materials could result in equipment not being available to
function during design events such as response to a seismic event.
Significance: The inspectors assessed the significance of the finding using Inspection
Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,
2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination
Process for Findings At-Power, Exhibit 4, External Events Screening Questions, the
inspectors determined the finding was of very low safety significance (Green) because the
finding is a deficiency affecting the design or qualification of a mitigating system, structure, or
component (SSC), but the SSC maintained its operability.
Cross-cutting Aspect: The inspectors determined that the performance deficiency occurred
more than three years ago and was not indicative of current performance.
Enforcement:
Violation: Title 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, requires, in part, that activities affecting quality shall be accomplished in
accordance with documented instructions, procedures, or drawings, of a type appropriate to
the circumstances. Procedure ECE-6.02-03, Critical Characteristics Development, an
Appendix B quality related procedure, provides instructions for the commercial grade
dedication of materials and parts.
Contrary to the above, in 2003 when upgrading the safety classification of Ashcroft series 200
diaphragms to safety related, the licensee failed to accomplish activities affecting quality in
accordance with documented instructions, procedures, or drawings, of a type appropriate to
the circumstances. Specifically, the licensee failed to follow the requirements of procedure
ECE-6.02-03 when upgrading the safety classification of material.
Disposition: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
Failure to Incorporate Design Information Into System Test Procedures
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Mitigating
Systems
Green
Closed
None
71152 -
Problem
Identification
and
Resolution
The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B, Criterion XI,
Test Control, for the licensees failure to ensure that station test procedures incorporated all
requirements contained in applicable design documents. Specifically, the stations test
procedures for the component cooling water system failed to test the safeguards loops supply
and return train isolation valves for leakage. Excess leakage from these valves could prevent
the performance of a safety function.
Description: During fill and vent activities on the B train safeguards loop of the Unit 1
component cooling water system on October 24, 2017, the licensee noted a system pressure
rise and determined the cause to be leakage past safeguards loops train A and B isolation
valves 1-HV-4513 and 1-HV-4515 (respectively). The component cooling water system has
four valves that close on an empty level in the surge tank to separate the safeguards loops
from each other and from the non-safeguards loop. The licensee initiated Condition Report
CR-2017-011897 to capture this issue in the stations corrective action program.
The inspectors reviewed this condition report and noted that the licensee had determined that
the leakage past the valves was approximately 40.3 gallons per minute (gpm). Inspectors
noted that this exceeded the allowable leakage limit of 37 gpm and the licensee had
performed an operability determination and determined that the valves were operable but
degraded based on an engineering evaluation. During their review of the operability
evaluation, the inspectors noted the following:
Makeup to the surge tank is normally an automatic function; however, during events
that result in a loss of instrument air, automatic makeup to the surge tank is lost and
manual makeup is required but not assumed to start for 30 minutes following receipt of
the empty alarm.
When the surge tank reaches the empty level setpoint, this causes safeguards
loops supply and return train isolation valves 1-HV-4512, 1-HV-4514, 1-HV-4513,
and 1-HV-4515 to close which separates the safeguards loops from each other
and isolates them from the non-safeguards loop fast enough to prevent loss of
inventory from at least one of the safeguards loops.
The surge tank design analysis assumes a system leak rate of 1 gpm (0.4 gpm for
Unit 2).
Safeguards loop supply and return isolation valve design stroke time is 45 seconds.
Worst case break is in the non-seismic piping in the non-safeguards loop (seismic
event will result in a loss of offsite power which stops automatic makeup to the surge
tank).
Therefore, based on the operator response time and system leak rate the allowable
train leakage limit is 37 gpm [10 gpm for Unit 2]. This ensures that there is adequate
volume in the surge tank below the empty level to accommodate the water
depletion due to postulated line break in the non-safeguard loop or the opposite
train during the closing time of the isolation valves, without depleting the tank
volume.
The licensee used measured stroke time of the valves, 27 seconds for both valves, as
the assumed closing time and determined that the allowed train leakage was 46 gpm.
Inspectors also noted that previously the licensee had experienced a similar issue.
Specifically, on May 15, 2016, during train A restoration activities, the licensee identified that
train A and B isolation valves 1-HV-4512 and 1-HV-4514 (respectively) were leaking by at
approximately 43.55 gpm.
Inspectors questioned how the licensee was monitoring the system for leakage and queried
the licensee about what testing is done on the system. The licensee responded that walk
downs were done looking for leakage. Inspectors asked if the licensee performed train
leakage test since the supply and return isolation valves were potential leak paths that could
not be identified by walk down. The licensee responded that no testing looking for leaks was
conducted, nor did the licensee believe they were required to do so.
However, following a review of the stations Updated Final Safety Analysis Report, Chapters 3
and 9, the inspectors determined that:
The component cooling water system and its safeguards loop components are
required to withstand the effects of natural phenomena, such as seismic events,
without loss of capability to perform its safety function [remove heat from safeguards
loop components]. Therefore, one of the safeguards loops of the component cooling
water system is required to remain operational during and following a failure of a
non-seismic component in the non-safeguards loop following a seismic event
assuming a single failure in the other loop [makes that loop unavailable].
The closure time of the safeguards loop isolation valves and the train leakage limit
are design requirements since they affect the ability of the system to perform its
safety function.
Further, Title 10 CFR 50, Appendix B, Criterion XI requires, in part, that a test program shall
be established to assure that all testing required to demonstrate that structures, systems, and
components will perform satisfactorily in service is identified and performed in accordance
with written test procedures which incorporate the requirements and acceptance limits
contained in applicable design documents.
Based on this, inspectors determined that the licensees practice of walking down the
component cooling water system looking for leakage was not adequate and that the licensee
should be testing the safeguards loops for leakage since leakage past the loop isolation
valves could prevent the system from performing its safety function. Inspectors determined
that this was applicable to both units.
Inspectors determined that this issue did not represent current performance because the
licensee had not reviewed nor revised the testing methodology for the system in the last three
years.
Corrective Action(s): The licensee performed an operability determination that established a
reasonable expectation of operability pending development of additional corrective actions.
Corrective Action Reference(s): Condition Report CR-2017-012024
Performance Assessment:
Performance Deficiency: The licensees failure to incorporate design information into system
test procedures was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor
because it adversely affected the equipment performance attribute of the Mitigating Systems
cornerstone and adversely affected the cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent undesirable
consequences. Specifically, not monitoring for system leakage could result in a leak rate that
would prevent the performance of system safety function.
Significance: The inspectors assessed the significance of the finding using Inspection
Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,
2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination
Process for Findings At Power, Exhibit 2, Mitigating Systems Screening Questions, the
inspectors determined the finding was of very low safety significance (Green) because: (1) it
was not a design deficiency; (2) it did not represent a loss of system and/or function; (3) it did
not represent an actual loss of function of at least a single train for longer than its technical
specification allowed outage time; and (4) it did not result in the loss of a high safety
significant nontechnical specification train.
Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the
performance deficiency was not reflective of current performance.
Enforcement:
Violation: Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that
a test program shall be established to assure that all testing required to demonstrate
components will perform satisfactorily in service is identified and performed in accordance
with written procedures which incorporate the requirements and acceptance limits contained
in applicable design documents.
Contrary to the above, from initial construction until present, the licensee failed to established
a test program to assure that all testing required to demonstrate components will perform
satisfactorily in service is identified and performed in accordance with written procedures
which incorporate the requirements and acceptance limits contained in applicable design
documents. Specifically, the licensee failed to incorporate design information into system test
procedures for the component cooling water system relative to leak testing for the safeguards
loops supply and return train isolation valves.
Disposition: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
Failure to Provide Adequate Procedure
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Mitigating
Systems
Green
Closed
None
71152 -
Problem
Identification
and
Resolution
The inspectors identified a Green, non-cited violation of Technical Specification (TS) 5.4.1,
Procedures, associated with the licensees failure to provide procedures appropriate to the
circumstances. Specifically, station procedure INC-2085, Rework and Replacement of I&C
Equipment, did not contain adequate instructions for wiring current-to-pressure (I/P)
converters for safety related components which resulted in the steam generator atmospheric
relief valve I/P converters being placed in a seismically unqualified configuration.
Description: On October 24, 2017, it was reported to the control room that steam generator
2-03 atmospheric dump valve 2-PV-2327 was leaking. The valve was found to be open
approximately 20 percent. This issue was entered into the corrective action program as
Condition Report CR-2017-011922. During the licensees investigation they noted that work
had been going on in the vicinity of the I/P converter for valve 2-PV-2327 and that
maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold
pole. The licensee also found that the I/P converter output settings were high. When the
licensee removed the cover of the converter they discovered that excess lead wires stored in
the housing were in contact with moveable parts of the converter which caused valve 2-PV-
27 to open. The licensee moved the lead wires so they were no longer in contact with the
moveable parts of the I/P converter.
Subsequently, on October 30, 2017, operators noted that steam generator 1-03 atmospheric
dump valve 1-PV-2327 was not indicating fully shut as demanded. The valve was found to be
open approximately 20 percent. This issue was entered into the corrective action program as
Condition Report CR-2017-012141. During the licensees investigation they noted that work
had been going on in the vicinity of the I/P converter for valve 1-PV-2327 and that
maintenance workers had inadvertently struck the housing for the I/P converter with a scaffold
pole. The licensee also found that the I/P converter output settings were high. When the
licensee removed the cover of the converter they discovered that excess lead wires stored in
the housing were in contact with moveable parts of the converter which caused
valve 1-PV-2327 to open. The licensee moved the lead wires so they were no longer in
contact with the moveable parts of the I/P converter.
The licensee performed an equipment cause analysis checklist and determined that
inadequate work practices was the cause of the issues. Inspectors questioned the licensees
identified cause in that that both issues appeared to happen after the housing for the
converters was struck with a scaffold pole, and raised concerns regarding seismic
qualification of the converters.
These concerns were expressed to the licensee who subsequently determined that the
excess wiring in the converter housing was not in a qualified seismic configuration. The
licensee determined that this configuration had existed most likely since initial installation of
the I/P converters and this was due to inadequate guidance provided in station procedure
INC-2085, Rework and Replacement of I&C Equipment, for maintenance personnel
regarding proper storage of excess field leads. Specifically, the procedure did not provide
sufficient guidance to ensure that electrical lead wire or other components within the I/P
converter were sufficiently secured to preclude contact with the moveable parts of the I/P
converter, in order to ensure the function and seismic qualification of the components were
maintained.
Corrective Action(s): The licensee performed an operability determination that established a
reasonable expectation of operability, developed work orders to remove the excess wiring
from the converters, and changed procedure INC-2085 to not allow excess wiring in the
converter housing.
Corrective Action Reference(s): Condition Report CR-2017-011922
Performance Assessment:
Performance Deficiency: The licensees failure to prescribe adequate procedures to perform
quality related activities associated with the steam generator atmospheric relief valve I/P
converters was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor
because it adversely affected the equipment performance attribute of the Mitigating Systems
cornerstone and adversely affected the cornerstone objective to ensure the availability,
reliability, and capability of systems that respond to initiating events to prevent undesirable
consequences. Specifically, the improper training of the lead wires resulted in the I/P
converters being in a non-seismically qualified configuration.
Significance: The inspectors assessed the significance of the finding using Inspection
Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated
October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance
Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening
Questions, the inspectors determined the finding was of very low safety significance (Green)
because: (1) it was not a design deficiency; (2) it did not represent a loss of system and/or
function; (3) it did not represent an actual loss of function of at least a single train for longer
than its technical specification allowed outage time; and (4) it did not result in the loss of a
high safety significant non-technical specification train.
Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the
performance deficiency was not reflective of current performance.
Enforcement:
Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be
established, implemented, and maintained covering the applicable procedures recommended
in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33,
Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-
related equipment be performed in accordance with written procedures appropriate to the
circumstances.
Contrary to the above, from initial installation through March 13, 2018, for maintenance
activities on steam generator atmospheric relief valve I/P converters, an activity that can
affect the performance of safety-related equipment to which Technical Specification 5.4.1.a
applies, the licensee failed to assure that the maintenance procedures were appropriate to
the circumstances.
Disposition: This violation is being treated as a Non-Cited Violation, consistent with
Section 2.3.2 of the Enforcement Policy.
Inadequate Maintenance Procedure for Feedwater Valves
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Green
Closed
None
71153 -
Follow-up of
Events and
Notices of
Enforcement
Discretion
The inspectors reviewed a self-revealed, Green non-cited violation of TS 5.4.1, Procedures,
associated with the licensees failure to prescribe adequate procedures for performing
maintenance on the feedwater bypass control valves. Specifically, the licensees procedure
failed to specify the correct torque on the hand wheel screw locknut, resulting in a loose
locknut which led to a control valve failure and a turbine trip.
Description: During the Unit 2 startup on August 11, 2017, following a forced outage, a
turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main
generator on the grid. The turbine trip and initiation of auxiliary feedwater was caused by
steam generator 2-02 water level rising above the high level setpoint due to a failure of the
steam generator 2-02 feedwater bypass control valve 2-LV-2163 to close on demand. These
valves are equipped with a valve hand wheel locknut designed to prevent the manual hand
wheel from rotating due to vibration. The valve failed to close because the valve hand wheel
locknut had backed off its normal fully closed position allowing the manual hand wheel to
rotate open and preventing the valve from closing. The licensee performed a review of work
history on the valve and identified work activities during which the locknut was manipulated.
The licensee determined that the locknut was last manipulated during replacement of the
2-LV-2163 elastomers on October 15, 2015. The work was done in accordance with
MSM-C0-6602, Fisher Diaphragm Actuator Maintenance, Section 8.5. The guidance in
MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN hand wheel screw locknut, but
does not include specific acceptance criteria or guidance on the required torque to apply
when tightening. For comparison, MSM-C0-6602 section 8.4 also includes a step to tighten
the locknut, but states TIGHTEN hand wheel screw locknut snug tight. The phrase snug
tight is used by licensee maintenance personnel to denote a qualitative torque value to apply
to a component to ensure it will not come loose during normal operation. The licensee
determined that the locknut needed to be left snug tight, and that the guidance in section 8.5
was not adequate. The inspectors determined that the inadequate procedural guidance had
existed in the procedure since October 2007.
Inspectors determined that the failure of steam generator 2-02 feedwater bypass control
valve 2-LV-2163 to close on demand was a significant condition adverse to quality because
this issue resulted in a turbine trip and initiation of auxiliary feedwater, and could have
resulted in a reactor scram
Corrective Action(s): The licensee verified all feedwater bypass control valve locknuts have
been properly tightened in accordance with the appropriate qualitative torque value of snug
tight.
Corrective Action Reference(s): CR-2017-009139
Performance Assessment:
Performance Deficiency: The licensees failure to prescribe adequate procedures to perform
quality related activities associated with the feedwater bypass control valves was a
performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor
because it adversely affected the procedure quality attribute of the Initiating Events
Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset
plant stability and challenge critical safety functions during shutdown as well as power
operations. Specifically, the inadequate procedure resulted in a failure of a feedwater bypass
control valve leading to an unplanned turbine trip and initiation of auxiliary feedwater.
Significance: The inspectors assessed the significance of the finding using Inspection
Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,
2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events
Screening Questions, the inspectors determined the finding was of very low safety
significance (Green) because it did not cause a reactor trip and the loss of mitigation
equipment relied upon to transition the plant to a stable shutdown condition.
Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the
performance deficiency was not reflective of current performance.
Enforcement:
Violation: Technical Specification 5.4.1.a states, in part, that written procedures shall be
established, implemented, and maintained covering the applicable procedures recommended
in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33,
Appendix A, Section 9.a, requires that maintenance that can affect the performance of safety-
related equipment be performed in accordance with written procedures appropriate to the
circumstances.
Contrary to the above, from October 2007 through August 2017, for maintenance activities on
the feedwater bypass control valves, an activity that can affect the performance of safety-
related equipment to which Technical Specification 5.4.1.a applies, the licensee failed to
assure that the maintenance procedures were appropriate to the circumstances.
Disposition: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
Failure to Correct a Significant Condition Adverse to Quality
Cornerstone
Significance
Cross-cutting
Aspect
Report
Section
Green
Closed
P.2 - Problem
Identification
and Resolution,
Evaluation
71153 -
Follow-up of
Events and
Notices of
Enforcement
Discretion
The inspectors identified a Green, non-cited violation of 10 CFR 50, Appendix B,
Criterion XVI, Corrective Action, associated with the licensees failure to take corrective
action to preclude repetition of a significant condition adverse to quality. Specifically, a
feedwater bypass control valve vibrated open resulting in a turbine trip and initiation of
auxiliary feedwater. The licensee determined that the cause was an inadequate procedure
for performing maintenance on the feedwater bypass control valves, but failed to correct the
inadequate procedure after identifying it as the cause of a control valve failure and a turbine
trip.
Description: During the Unit 2 startup on August 11, 2017, following a forced outage, a
turbine trip and initiation of auxiliary feedwater occurred when attempting to place the main
generator on the grid (refer to NCV 05000445/2018001-04; 05000446/2018001-04 above).
The turbine trip and initiation of auxiliary feedwater was caused by steam generator 2-02
water level rising above the high level setpoint due to a failure of the steam generator 2-02
feedwater bypass control valve 2-LV-2163 to close on demand. Inspectors determined that
this was a significant condition adverse to quality because this issue resulted in a turbine trip
and initiation of auxiliary feedwater, and could have resulted in a reactor scram.
The licensee determined that the valve failed to close because the valve hand wheel locknut
had backed off its normal fully closed position, preventing the valve from closing. The
licensee performed a cause evaluation and identified that MSM-C0-6602, Fisher Diaphragm
Actuator Maintenance, contained inadequate guidance for restoration of the valve following
maintenance. The guidance in MSM-C0-6602 section 8.5, step 8.5.43 states to TIGHTEN
hand wheel screw locknut, but does not include specific acceptance criteria or guidance on
the required torque to apply when tightening. Section 8.5 is used to perform elastomer
replacement on these valves and was last used on 2-LV-2163 during replacement of the
elastomers on October 15, 2015. Although the procedure contained inadequate guidance in
section 8.5, the procedure also contains a section for general reassembly of the valve. MSM-
C0-6602 section 8.4 includes a step to tighten the locknut, but states TIGHTEN hand wheel
screw locknut snug tight. The phrase snug tight is used by licensee maintenance
personnel to denote a qualitative torque value to apply to a component to ensure it will not
come loose during normal operation. The licensee, in developing their corrective action plan,
conflated section 8.4 and 8.5 and erroneously credited the correct step in section 8.4 as a
corrective action for the inadequate step in section 8.5. The licensee assumed the corrective
action had been completed during a procedural revision in 2012, and closed the corrective
action plan without correcting section 8.5.
The inspectors reviewed the cause evaluation and corrective actions and identified that the
licensee had failed to correct the inadequate procedure. The inspectors determined that
MSM-C0-6602 section 8.5, step 8.5.43 was not revised, and no action was planned to revise
it. The inspectors determined this to be a result of the licensees cause evaluation failing to
identify the specific inadequate procedural step that caused the failure and as a result did not
correct the deficiency.
The inspectors determined that the licensee had failed to implement corrective actions to
preclude repetition of a significant condition adverse to quality.
Corrective Action(s): The licensee has verified all feedwater bypass control valve locknuts
have been properly tightened, and changed procedure MSM-C0-6602, Fisher Diaphragm
Actuator Maintenance, step 8.5.43 to require the locknut to be tightened snug tight.
Corrective Action Reference(s): CR-2018-000959
Performance Assessment:
Performance Deficiency: The licensees failure to implement corrective actions to preclude
repetition of a significant condition adverse to quality was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor
because it adversely affected the procedure quality attribute of the Initiating Events
Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset
plant stability and challenge critical safety functions during shutdown as well as power
operations. Specifically, the inadequate procedure could reasonably be expected to result in
another failure of the control valve and subsequent turbine trip.
Significance: The inspectors assessed the significance of the finding using Inspection
Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7,
2016, and Inspection Manual Chapter 0609, Appendix A, Exhibit 1, Initiating Events
Screening Questions, the inspectors determined the finding was of very low safety
significance (Green) because it did not cause a reactor trip and the loss of mitigation
equipment relied upon to transition the plant to a stable shutdown condition.
Cross-cutting Aspect: The finding was assigned a cross-cutting aspect of evaluation because
the licensee did not thoroughly evaluate issues to ensure that resolutions address causes and
extent of conditions commensurate with their safety significance. (P.2)
Enforcement:
Violation: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that,
for significant conditions adverse to quality, measures shall assure that the cause of the
condition is determined and corrective action taken to preclude repetition.
Contrary to the above, from August 2017 through February 2018, the licensee failed to
establish measures to assure corrective action was taken to preclude repetition of a
significant condition adverse to quality. Specifically, the licensee failed to correct the cause of
the event by correcting the inadequate maintenance procedure for the feedwater bypass
control valves.
Disposition: This violation is being treated as a non-cited violation, consistent with
Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
The inspectors confirmed that proprietary information was controlled to protect from public
disclosure.
On March 31, 2018, the inspectors presented the quarterly resident inspector inspection results
to Mr.
- T. McCool, Site Vice President, and other members of the licensee staff.
THIRD PARTY REVIEWS
Inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the
inspection period.
DOCUMENTS REVIEWED
7111112 - Maintenance Effectiveness
Condition Reports
CR-2016-009733
CR-2017-007811
CR-2016-010346
CR-2016-008375
CR-2003-000664
Procedures
(Number)
Title
Revision
Or Date
ECE-6.02-03
Critical Characteristics Development
5b
71152 - Problem Identification and Resolution
Condition Reports
CR-2017-012024
CR-2017-011897
CR-2016-004715
CR-2017-011922
CR-2017-012141
CR-2017-012144
CR-2018-000909
CR-2017-011944
CR-2018-002058
CR-2018-001629
Work Orders
3793710
3505655
3793738
3-01-330488-02
3-01-330490-02
3-01-332709-01
3-01-330492-02
4793333
5516071
5435660
20265
20201
25302
20253
Procedures
(Number)
Title
Revision
Or Date
MSM-C0-8837
Fisher Butterfly Valve Rework
ICA-101
I&C Work Control
INC-2085
Rework and Replacement of I&C Equipment
INC-4270A
Channel Calibration Power Relief Valve Control
Steam Generator 3 Channel 2327
Miscellaneous Documents
Number
Title
Revision
or Date
ME(B)-073
CCW Surge Tank Volume
SEQSP-MS-78-01
Fisher Air Operated Globe Valve Model 8X6 EWP
71153 - Follow-up of Events and Notices of Enforcement Discretion
Condition Reports
CR-2017-009139
CR-2018-000959
CR-2013-006702
CR-2017-005448
Procedures
(Number)
Title
Revision
Or Date
MSM-C0-6602
Fisher Diaphragm Actuator Maintenance
4