IR 05000324/2022002
| ML22216A254 | |
| Person / Time | |
|---|---|
| Site: | Brunswick |
| Issue date: | 08/05/2022 |
| From: | Matthew Fannon NRC/RGN-II/DRP/RPB4 |
| To: | Krakuszeski J Duke Energy Progress |
| References | |
| IR 2022002 | |
| Download: ML22216A254 (16) | |
Text
SUBJECT:
BRUNSWICK STEAM ELECTRIC PLANT - INTEGRATED INSPECTION REPORT 05000324/2022002 AND 05000325/2022002
Dear Mr. Krakuszeski:
On June 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Brunswick Steam Electric Plant. On July 20, 2022, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Matthew S. Fannon, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket Nos. 05000324 and 05000325 License Nos. DPR-62 and DPR-71
Enclosure:
As stated
Inspection Report
Docket Numbers: 05000324 and 05000325
License Numbers: DPR-62 and DPR-71
Report Numbers: 05000324/2022002 and 05000325/2022002
Enterprise Identifier: I-2022-002-0016
Licensee: Duke Energy Progress, LLC
Facility: Brunswick Steam Electric Plant
Location: Southport, NC
Inspection Dates: April 01, 2022 to June 30, 2022
Inspectors: C. Curran, Resident Inspector A. Rosebrook, Senior Reactor Analyst M. Schwieg, Senior Reactor Inspector J. Seat, Senior Project Engineer G. Smith, Senior Resident Inspector J. Steward, Senior Resident Inspector
Approved By: Matthew S. Fannon, Chief Reactor Projects Branch 4 Division of Reactor Projects
Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Brunswick Steam Electric Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Unit 1 began the period shutdown for a refueling outage. On April 2, 2022, the reactor was taken critical and a plant startup was commenced. On April 4, the main generator output breaker was closed and a power ascension was commenced. On April 5, power was stabilized at 30 percent rated thermal power (RTP) in order to perform condenser dimple plug testing to locate leaking water-box tubes. Following completion of dimple plug testing, a power ascension was commenced and Unit 1 reached 100 percent (full) RTP on April 15 following two rod improvements. Unit 1 continued to operate at full RTP until April 19 when power was reduced to 96 percent RTP due to a failure of a cell in the variable frequency drive (VFD) associated with the 'B' recirculation pump motor. Following the bypass of the 1B2 cell in the 'B' VFD, Unit 1 was restored to full RTP on the same day and continued to operate there until May 19 when power was reduced to 80 percent RTP due to a loss of one of the four Unit 1 off-site power lines (Weatherspoon). Following repairs to the Weatherspoon line, Unit 1 was restored to full RTP on May 21 and continued to operate at or near full RTP for the remainder of the inspection period.
Unit 2 began the period at full RTP and operated there until May 7, when power was reduced to 70 percent RTP in order to insert a second suppression rod due to an existing fuel leak. Following insertion of a second suppression rod, Unit 2 was restored to full power on May 8 and continued to operate there until May 20 when power was reduced to 70 percent RTP for the purpose of performing a control rod sequence exchange as well as insert a third suppression rod. Following the sequence exchange and suppression rod insertion, Unit 2 was restored to full RTP on May 25 following one rod improvement. Unit 2 continued to operate at or near full RTP for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
- (1) From April 12 through April 14, 2022, the inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal high temperatures for the following systems:
offsite AC power systems and onsite alternate AC systems, including the switchyard and transformers
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) 2C and 2E main control room (MCR) heating, ventilating, air conditioning (HVAC)units while the 1D MCR HVAC unit was out-of-service (OOS) for replacement on April 26, 2022
- (2) Unit 2 high pressure coolant injection (HPCI) system while the Unit 2 reactor core isolation cooling system was OOS for planned maintenance on April 26, 2022
- (3) Unit 2 nuclear service water and conventional service water (CSW) while Unit 2 'B' CSW pump was OOS for planned maintenance on May 11, 2022
- (4) Unit 2 B residual heat removal (RHR) train while A train was OOS for planned maintenance on May 25, 2022
- (5) emergency diesel generators (EDGs) -2, -3, and -4 while EDG-1 was OOS for a maintenance outage on June 22, 2022
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Fire area RB2-01-D in the Unit 2 southeast RHR room on April 14, 2022
- (2) Control building HVAC room on April 26, 2022
- (3) 1A, 1B, 2A, 2B battery rooms in the 23 elevation of the control building on May 5, 2022
- (4) Unit 1 reactor building -17 elevation on May 5, 2022
- (5) Service water building 20 and 4 elevations on May 10, 2022
- (6) Unit 1 reactor building 20 elevation on May 11, 2022
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the onsite fire brigade training and performance during announced fire drills conducted on May 18, 2022, in the service building HVAC room and on May 24, 2022, in the insulator shop (yard area).
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)
The inspectors evaluated internal flooding mitigation protections in the:
- (1) safety-related manholes (NS3, NS2, 5NW) on April 21, 2022
- (2) emergency diesel generator building and 4-day fuel oil tank rooms on May 18, 2022
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the control room during Unit 1 reactor startup on April 2, 2022.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)
- (1) The inspectors observed and evaluated two operating crews during a simulator exam on April 21, 2022. The simulator exam was part of the licensed operator continuing training cycle 2. The scenario consisted of a recirculation loop flow transmitter failure, a reactor building closed cooling water heat exchanger leak, a loss of off-site power, and a small break loss of coolant accident.
- (2) On May 19, 2022, the inspectors completed a review and evaluation of a written exam given in licensed operator continuing training cycle 1 conducted during the first quarter of 2022.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (2 Samples)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
- (1) relay failure (high contact resistance) that resulted in a spurious partial Group 6 and secondary containment isolation (NCR 2410783) on January 4, 2022
- (2) EDG-1 maintenance outage conducted from June 20 through June 29, 2022
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) emergent failure of reactor building radiation monitor on April 14, 2022
- (2) emergent steam leak in the Unit 2 main steam isolation valve (MSIV) pit discovered on May 8, 2022
- (3) elevated risk due to 2B CSW pump strainer planned maintenance from May 9 through May 12, 2022
- (4) emergent failure of 1C CSW pump strainer shear pin on May 11, 2022
- (5) elevated risk due to Unit 1 A train RHR outage on May 25, 2022
- (6) elevated risk due to EDG-1 maintenance outage on June 23, 2022
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) 2-B32-F031B actuator rating exceeded (NCR 2414157)
- (3) deterioration of concrete wall in Unit 2 reactor building (NCR 2305749)
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
- (1) control building HVAC modification (Engineering Change 417875) completed on June 16, 2022
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)
The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:
- (1) 0PT-09.2 HPCI operability test after replacement of the flow controller FIC-R600 in accordance with (IAW) work order (WO) 20304709
- (2) 2B standby gas treatment system (SBGT) system following planned maintenance to replace drain piping IAW WO 20372477
===20377862
- (5) 0PT-09.2, HPCI operability test following replacement of the Unit 2 HPCI EGR servo motor IAW WO 20525661
- (6) G31-F001, reactor water cleanup (RWCU) inboard suction valve following valve replacement IAW WO 20377862
- (7) G31-F004, RWCU outboard suction valve following valve replacement IAW WO 20377862
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01)===
- (1) The inspectors evaluated Unit 1 refueling outage (B1R24) activities from March 5, 2022 to April 4, 2022, when the main generator was synched to the grid.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:
Surveillance Tests (other) (IP Section 03.01) (1 Sample)
- (1) Loss of offsite power/loss of coolant accident (LOOP/LOCA) test on April 7, 2022
Inservice Testing (IP Section 03.01) (1 Sample)
- (1) Unit 2 'B' RHR quarterly surveillance on June 4, 2022
RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)
- (1) Unit 1 reactor coolant system (RCS) leakage IAW 0OI-02.3, "Drywell Leakage Control," on June 30, 2022
71114.06 - Drill Evaluation
Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)
The inspectors evaluated:
- (1) A simulator examination (training evolution) given to two separate operating crews on April 22, 2022. The simulator examination included a drill/exercise performance opportunity.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04)===
- (1) Unit 1 (April 1, 2021 through March 31, 2022)
- (2) Unit 2 (April 1, 2021 through March 31, 2022)
MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)
- (1) Unit 1 (April 1, 2021 through March 31, 2022)
- (2) Unit 2 (April 1, 2021 through March 31, 2022)
MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)
- (1) Unit 1 (April 1, 2021 through March 31, 2022)
- (2) Unit 2 (April 1, 2021 through March 31, 2022)
===71152A - Annual Follow-up Problem Identification and Resolution
Annual Follow-up of Selected Issues (Section 03.03)===
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) NCR 2379462: Reactor recirculation pump seal premature failure
71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)
- (1) The inspectors reviewed the licensees corrective action program for potential adverse trends in operations and maintenance that might be indicative of a more significant safety issue.
INSPECTION RESULTS
Observation: Reactor Recirculation Pump Seal Premature Failure 71152A The inspectors conducted a detailed review of NCR 2379462, Reactor Recirculation Pump Seal Premature Failure. The inspectors chose this sample because it dealt with the barrier integrity cornerstone involving the recirculation pump seals. On February 15, 2021, the second stage seal of the Unit 2 'B' recirculation pump was noted to be degrading. Based on the rate of degradation, the decision was made to replace the seal package during the upcoming March 2021 refueling outage. Following replacement of both the 'A' and 'B' seal packages during the refueling outage, operators noted a similar degrading second stage seal on the Unit 1 'B' recirculation pump on April 19, 2021. The decision was made to enter a maintenance outage on April 30 as the rate of seal degradation was excessive and the seal would not last until the next refueling outage in March 2022. The recirculation pump seals have an expected life of six years, yet the inspectors observed that the seals are degrading prior to reaching the end of their expected life cycle.
The licensee performed a detailed root cause analysis in order to understand the failure mechanism and develop corrective actions to address the deficiencies. The root cause was determined to be self-induced electro-corrosion of the second stage secondary seal.
Several corrective actions have been implemented including the replacement of all 4 seals on both units. The inspectors noted that this will be a long-term effort as the design changes to address the direct cause of the electro-corrosion are still being developed. The inspectors determined that the licensees plan to address this issue was reasonably commensurate with the safety significance of the equipment that might be affected by this type of equipment failure.
Observation: Semi-Annual Trend Review 71152S The inspectors performed a trend analysis on the licensees corrective action program to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on equipment performance trends, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of January
- June 2022, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends.
Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions.
During this review, the inspectors noted the reemergence of a negative trend with respect to reactor fuel performance. In Brunswick inspection report 05000324/2019002 and 05000325/2019002 (ADAMS Accession No. ML19221B744), the inspectors noted a negative trend based on three separate fuel cycles experiencing fuel failures. Following these failures, the licensee aggressively addressed the failures by performing detailed root cause evaluations. No definitive cause was noted. However, some of the failures were attributed to potential negative effects from foreign material. Additionally, one failure was attributed to a manufacturing defect. In order to address the foreign material, the license chose to clean all fuel assemblies during the upcoming refueling outages as well as perform a foreign object search and retrieval (FOSAR) activity. As of June 30, 2022, the fuel cleaning and FOSAR activities have been completed on both Unit 1 and Unit 2 during the most recent refueling outages. Since the initial determination of a negative trend in 2019, the inspectors noted two more cycles (Unit 1 in 2020 and Unit 2 in 2022) where fuel failures were encountered.
Despite the fuel cleaning and FOSAR efforts, Unit 2 recently experienced another fuel failure in April 2022 which necessitated flux suppression. Even given the flux suppression, the Unit 2 reactor coolant system activity has remained elevated. In summary, the condition reports (CRs) noted below document that five of the past seven fuel cycles on Unit 1 and Unit 2 experienced fuel leaks. Fuels leaks typically drive the licensee to suppress the neutron flux of the affected fuel assembly by inserting control rod(s) in the vicinity of the fuel leak. The inserted control rod can result in reduction of margin to thermal limits, limit rates of power increase, and increase the number of rod programming changes. The inspectors discussed this negative trend with the licensee.
- CR 2416401 (Unit 2, 2022)
- CR 2323829 (Unit 1, 2020)
- CR 2276790 (Unit 1, 2019)
- CR 2176522 (Unit 2, 2018)
- CR 2078244 (Unit 1, 2016)
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On July 20, 2022, the inspectors presented the integrated inspection results to John A.
Krakuszeski and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.01 Miscellaneous SD-50 230 KV Electric Distribution System 01/14/2020
Procedures CSD-EG-ALL-Nuclear Switchyard Operating Guidelines 08/30/2018
2000.2
71111.04 Miscellaneous SD-37 Control Building Heating, Ventilation, and Air-Conditioning 16
System
SD-39 Emergency Diesel Generators 22
Procedures 0OP-37 Control Building Ventilation System Operating Procedure 75
0OP-39 Diesel Generator Operating Procedure 198
2OP-17 Residual Heat Removal System Operating Procedure 185
2OP-19 High Pressure Coolant Injection System Operating 147
Procedure
2OP-43 Service Water System Operating Procedure 175
SD-17 Residual Heat Removal System 20
SD-19 High Pressure Coolant Injection (HPCI) System 25
SD-43 Service Water System 27
71111.05 Engineering 288259 Seismic Verification of Fire Protection Piping 05/18/2022
Changes
Fire Plans CSD-BNP-PFP-Control Building Pre-Fire Plans 5
0CB
CSD-BNP-PFP-Miscellaneous Buildings Pre-Fire Plans - Protected Area 1
0MBPA
CSD-BNP-PFP-Power Block Auxiliary Areas Pre-Fire Plans (SW, RW, AOG, 4
Miscellaneous 0FPP-031 Fire Brigade Staffing Roster and Equipment Requirements 34
18-F-OS-01 Insulator Shop Fire Drill Scenario Guide 05/18/2022
21-F-SB-01 Service Building Air HVAC Room Fire Drill Scenario Guide 05/18/2022
Procedures 0AOP-13.0 Operation During Hurricane, Flood Conditions, Tornado, or 73
0PFP-013 General Fire Plan 55
0PLP-01.2 Fire Protection System Operability, Action, and Surveillance 51
Requirements
AD-EG-ALL-1520 Transient Combustible Control 13
Inspection Type Designation Description or Title Revision or
Procedure Date
CSD-BNP-PFP-Reactor Building Prefire Plans 2
1RB
71111.06 Corrective Action 555550 Fire Protection Piping Seismic Support Documentation 05/17/2022
Documents AS 681677-05 Assignment Summary 07/29/2019
Corrective Action 20537521 Work Order 05/19/2022
Documents
Resulting from
Inspection
Engineering DBD-144 External and Internal Flooding Topical Design Basis 1
Evaluations Document
PS-FP-G008 Analysis to Seismically Qualify Select Fire Protection Pipe 0
Supports in the Diesel Generator Building
Miscellaneous BNP-12-0104 Long Range Plan 05/18/2022
UFSAR section Diesel Generator Building Internal Flooding Protection 27
3.4.2.2
Work Orders 20335906 02 BNP Man Hole Inspection AD-EG-ALL-1214 05/24/2021
20449286 02 (LR) FOUR YEAR MAN HOLE INSPECTION PER AD-EG- 02
BNP-1214
20449286 02 INSPECT MAN HOLE, DOCUMENT EGR-NGGC-0351 02
INSPECTION
20449286 02 BNP Man Hole Inspection AD-EG-BNP-1214 10/11/2021
71111.11Q Miscellaneous LORX-202 Simulator Guide - Recirculation Loop 'A' flow transmitter 10b
failure, RBCCW high radiation, LOOP, Small Break LOCA
Segment 22-1 LOCT examination 2022 Cycle 1 01/13/22
Version A
Segment 22-1 LOCT Examination 2022 Cycle 1 01/19/22
Version B
Procedures 0GP-02 Approach to Criticality and Pressurization of the Reactor128
71111.12 Procedures AD-EG-ALL-1210 Maintenance Rule Program 3
AD-WC-ALL-ON-LINE WORK MANAGMENT 20
200
AD-WC-ALL-WORK IMPLEMENTATION AND COMPLETION 15
250
71111.13 Corrective Action 2426363 Unit 2 MSIV Pit Steam Leak 05/09/2022
Inspection Type Designation Description or Title Revision or
Procedure Date
Documents
Procedures 0AP-025 BNP Integrated Scheduling 60
AD-OP-ALL-0201 Protected Equipment 9
AD-WC-ALL-On-Line Work Management 20
200
AD-WC-ALL-Work Implementation and Completion 15
250
AD-WC-ALL-Work Activity Integrated Risk Management 13
0410
Work Orders 20225913 2-MS-F038D-MO, Backseat Valve Potential MSIV Pit Steam 05/10/2022
Leak
71111.15 Calculations 0HPCI-0011 HPCI RESPONSE TIME REQUIREMENT 002
Corrective Action Action Request: 2-B32-F031B Actuator Rating Exceeded 01/31/2022
Documents 02414157
Action Request: RHR Valve Weight Analysis Discrepancy 02/23/2022
2417296
Corrective Action 20226189 Work Request to drive repairs noted during inspection of the 05/12/2022
Documents Unit 1 South Core Spray Room EL -17'
Resulting from 2427216 1-RB1-BLG-EL-17-1 Cosmetic Defect on Unit 1 SCE 05/12/2022
Inspection Concrete Columns
Drawings 9527-F-02501 Unit 1 Reactor Building Plan Below Grade EL (-) 17' - 0" 29
General Arrangement
F-01230 Unit 2 Reactor Building Concrete Plan EL 20' - 0" - West 16
Engineering A/R 02423550 50.59 Screen to Extend HPCI Response Time Rev 00
Evaluations A/R 02423553 10 CFR 50.59 Evaluation to extend HPCI response time Rev 00
Operability 2305749 Repair Cosmetic Defect Void in Unit 2 Drywell Exterior Wall05/12/2022
Evaluations AD-OP-ALL-0105 OPERABILITY DETERMINATIONS 6
Procedures 0SPP-CEM500 Installation of Concrete and Grout 25
AD-OP-ALL-0105 Operability Determinations 6
71111.18 Engineering EC 417875 50.59 Screen for EC 417875 Rev 00
Changes EC 417875 CB HVAC Condensing Unit 1D Replacement Rev 015
Engineering A/R 2391929 50.59 Screen for EC 417875 Rev 00
Evaluations
Inspection Type Designation Description or Title Revision or
Procedure Date
Procedures PD-EG-ALL-1130 Engineering Change Program Rev 1
71111.19 Corrective Action 2426126 1-E41-V6 Flow Inst Connection Spraying Leak 05/05/2022
Documents
Resulting from
Inspection
Procedures 0PLP-20 Post-Maintenance Testing Program 55
- R.P. Adams Self-Cleaning Strainers, Model VWS 10 through 37
0PT-09.2 HPCI System Operability Test 153
Work Orders 20304709 1-E41-FIC-R600, Replace Controller, HPCI Turb Flo Ind 05/03/2022
Controller
20372477 2B SBGT Drain Line Repairs 05/16/2022
20377862 Recoat 1A SBGT Drain Line Piping 05/20/2022
20399034, 2B CSW Strainer maintenance 05/20/2022
20412939
20525661-06 Unit 2 HPCI Servo Replacement 3/12/22
71111.20 Procedures 0GP-02 Approach to Criticality and Pressurization of the Reactor128
0GP-03 Unit Startup and Synchronization 98
0GP-04 Increasing Turbine Load to Rated Power 132
71111.22 Procedures 0OI-02.3 Drywell Leakage Control 9
0PT-08.2.2B LPCI/RHR SYSTEM OPERABILTIY TEST - LOOP B 110
0PT-12.1A No.1 Emergency Diesel Generator LOOP/LOCA Loading 11
Test
71114.06 Procedures AD-EP-ALL-002 NRC Regulatory Assessment Performance Indicator 7
Guideline Emergency Preparedness Cornerstone
AD-EP-ALL-0101 Emergency Classification 3
CSD-EP-BNP-EAL Wallchart (Both Hot and Cold) 4
0101-02
71151 Engineering BNP-MECH-BNP Mitigating System Performance Index Plant Basis 2
Evaluations MSPI Document
BNP-PSA-069 NRC Mitigating System Performance Index (MSPI) PRA 17
Input Document
71152A Procedures AD-PI-ALL-0100 Corrective Action Program 27
71152S Procedures AD-PI-ALL-0100 Corrective Action Program 27
14