IR 05000354/2015004
| ML16033A381 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 02/02/2016 |
| From: | Bower F L Reactor Projects Branch 3 |
| To: | Braun R Public Service Enterprise Group |
| BOWER, FL | |
| References | |
| IR 2015004 | |
| Download: ML16033A381 (37) | |
Text
February 2, 2016
Mr. Robert Braun President and Chief Nuclear Officer PSEG Nuclear LLC N09 P.O. Box 236 Hancocks Bridge, NJ 08038
SUBJECT: HOPE CREEK GENERATING STATION UNIT 1 INTEGRATED INSPECTION REPORT 05000354/2015004
Dear Mr. Braun:
On December 31, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Hope Creek Generating Station (HCGS). The enclosed inspection report documents the inspection results, which were discussed on January 14, 2016, with Mr. Paul Davison, Site Vice President of Hope Creek, and other members of your staff. NRC Inspectors examined activities conducted under your license as they relate to safety and ur license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. The inspectors documented one finding of very low safety significance (Green) in this report. This finding did not involve a violation of NRC requirements. Further, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy. If you contest the non-cited violation or the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at HCGS. In addition, if you disagree with the cross-cutting aspect assigned to any finding, or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at HCGS. In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the etter, its enclosure, and your response (if any) will be the and Management System (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/ Fred L. Bower, III, Chief Reactor Projects Branch 3 Division of Reactor Projects Docket No. 50-354 License No. NPF-57
Enclosure:
Inspection Report 05000354/2015004
w/Attachment:
Supplementary Information cc w/encl: Distribution via ListServ
SUMMARY
IR 05000354/2015004; 10/01/2015 12/31/2015; Hope Creek Generating Station; Operability Determinations and Functionality Assessments. This report covered a three-month period of inspection by the resident inspectors and announced inspections performed by regional inspectors. Inspectors identified one finding of very low safety significance (Green) and one licensee-identified violation which was determined to be of very low safety significance in this report. The licensee-identified violation was determined to be violation of NRC requirements. The significance of most findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using April 29, 2015. Cross-Cross-December 4, 2014. All violations of NRC requirements are February 4, 2015. The described in NUREG- 5.
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a Green finding because PSEG did not follow procedures to ensure that an identified condition adverse to quality (CAQ) was adequately evaluated, documented, and corrected. Specifically, PSEG identified a CAQ associated with a station blackout (SBO) design calculation used to justify the main control room (MCR) heat load during a loss of ventilation, but failed to adequately evaluate, document and correct the CAQ. This CAQ challenged the reasonable assurance of functionality of the MCR during an SBO event and required PSEG to complete a detailed technical evaluation (TE) to prove functionality was maintained. performing a detailed TE to ensure MCR temperatures during an SBO would not have exceeded a functionality limit, and initiating actions to ensure issues identifying a potential CAQ receive the appropriate screening by operators, engineering and management staff. PSEG also revised SBO procedures to ensure the proper electrical loads were included when required to be shed in the event of an SBO event. PSEG documented the issue in the corrective action program (CAP) as Notification (NOTF) 20704285. This finding was more than minor because it was associated with the human performance attribute of the Mitigating Systems cornerstone and adversely affected its objective to ensure the capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the potential existed for the analyzed MCR heat load to be exceeded, affecting the ability of the MCR to remain functional during an SBO event. Additionally, the finding was similar to IMC 0612, Appendix E, examples j and k, in that, a design engineering calculation error resulted in a condition where there was a reasonable doubt of operability of a structure, system, or component (SSC). The finding was screened Process (SDP) for Findings-at- 2, 2012. The finding screened as very low safety significance (Green) using Exhibit 2 for Mitigating Systems Screening Questions, because the finding is a deficiency affecting the design or qualification of a mitigating SSC, but the affected SSC maintains its operability and/or functionality. Specifically, the design calculation error was a CAQ that challenged the reasonable assurance of functionality of the MCR during an SBO event and required a TE to prove functionality of the MCR during an SBO event was maintained.
4 The inspectors determined this finding has a cross-cutting aspect in the area of Problem Identification and Resolution (PI&R), Evaluation, in that PSEG did not thoroughly evaluate the issue to ensure that resolutions address causes and extent of conditions, commensurate with its safety significance. Specifically, issues of concern need to be properly classified, prioritized, and evaluated according to their safety significance, and operability and reportability determinations are developed, when appropriate. In this case, PSEG did not properly classify or evaluate an identified CAQ per their procedures. [P.2] (Section 1R15)
Other Findings
A violation of very low safety significance that was identified by PSEG was reviewed by the CAP. This violation and corrective action tracking number are listed in Section 4OA7 of this report.
5
REPORT DETAILS
Summary of Plant Status The Hope Creek Generating Station began the inspection period starting up in Operational Condition 2 following an unplanned automatic reactor scram on September 28, 2015. The unit was synchronized to the grid on October 2, 2015. The unit was returned to 100 percent rated thermal power (RTP) on October 3, 2015. On November 3, 2015, operators reduced power to approximately 80 percent to support planned maintenance on the Red Lion offsite power line. Operators returned the unit to full RTP on November 11, 2015. On December 19, 2015, operators reduced power to approximately 60 percent to support planned turbine valve testing, control rod scram time testing, and control rod sequence exchange. Operators returned the unit to full power on December 20, 2015. The unit remained at or near full RTP for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
Readiness for Seasonal Extreme Weather Conditions
a. Inspection Scope
extremely low outside temperatures experienced the week of December 28, 2015. The inspectors reviewed the abnormal operating procedure, HC.OP-AB.MISC-responding to adverse weather conditions. The inspectors walked down the emergency diesel generators (EDGs) and the switchyard to ensure compliancweather procedures. The inspectors also verified that operator actions defined in Documents reviewed for each section of this inspection report are listed in the Attachment.
b. Findings
No findings were identified.
1R04 Equipment Alignment Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial walkdowns of the following systems: maintenance on October 16 Reactor core isolation cooling (RCIC) system on October 26 Remote shutdown panel on December 5 The inspectors selected these systems based on their risk-significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors reviewed applicable operating procedures, system diagrams, the updated final safety analysis report (UFSAR), technical specifications (TSs), work orders (WOs), notifications, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions. The inspectors also performed field walkdowns of accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies. The inspectors also reviewed whether PSEG staff had properly identified equipment issues and entered them into the CAP for resolution with the appropriate significance characterization.
b. Findings
No findings were identified.
1R05 Fire Protection Resident Inspector Quarterly Walkdowns
a. Inspection Scope
The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that PSEG controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.
Review of compensatory measure fire watch for 1PS15 panel power supply failure on October 19 EDG room on November 12 Instrument and service air equipment mezzanine area the week of November 22 Review of compensatory measures for fire water storage tank inspections during the week of November 30
b. Findings
No findings were identified.
1R06 Flood Protection Measures
Internal Flooding Review
a. Inspection Scope
The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to identify internal flooding susceptibilities for the site. The inspectors review focused on the EDG rooms. The inspectors verified the adequacy of equipment seals located below the flood line, floor and water penetration seals, and common drain lines. The inspectors also reviewed the CAP to determine if PSEG was identifying and correcting problems associated with both flood mitigation features and site procedures for responding to flooding.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
.1 Quarterly Review of Licensed Operator Requalification Testing and Training
a. Inspection Scope
The inspectors observed licensed operator annual operating simulator exam on October 14, which included a reactor water cleanup pump trip, a safety auxiliaries cooling system (SACS) pump trip, a loss of coolant accident, an anticipated transient without scram, a control rod drive system flow control valve failure, and a high pressure coolant injection (HPCI) pump start failure. The inspectors evaluated operator performance during the simulated event and verified completion of risk significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classification made by the shift manager and the TS action statements entered by the control room supervisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify and document crew performance problems.
b. Findings
No findings were identified.
.2 Quarterly Review of Licensed Operator Performance in the Main Control Room
a. Inspection Scope
The inspectors observed and reviewed unit startup activities on September 30 and October 2. The inspectors observed infrequently performed test or evolution briefings, pre-shift briefings, and reactivity control briefings to verify that the briefings met the Administrative Procedure OP-AA-vision 1. Additionally, the inspectors observed test performance to verify that procedure use, crew communications, and coordination of activities between work groups similarly met established expectations and standards.
b. Findings
No findings were identified.
.3 Licensed Operator Requalification Program
a. Inspection Scope
On November 17, one NRC region-based inspector conducted an in-office review of results of licensee-administered annual operating tests for 2015, for HCGS operators. The biennial requalification written examination was not administered in 2015. The inspection assessed whether Pass/Fail rates were consistent with the guidance of NRC rformance (individual or crew) did not exceed 20%.
1 out of 47 operators failed at least one section of the Annual Exam. The overall individual failure rate was 2.2%. 0 out of 19 crews failed the simulator test. The crew failure rate was 0%.
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on SSC performance and reliability. The inspectors reviewed system health reports, CAP documents, maintenance WOs, and maintenance rule basis documents to ensure that PSEG was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria established by PSEG staff was reasonable. As applicable, for structures, systems, and components classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these structures, systems, and components to (a)(2). Additionally, the inspectors ensured that PSEG staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.
Review of effluent radiation monitor system (RMS) scoping fuel pool cooling pump after significant oil loss was discovered on October 5
b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities listed below to verify that PSEG performed the appropriate risk assessments prior to removing equipment for work. The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that PSEG personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the assessments were accurate and complete. When PSEG performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of consistent with the risk assessment. The inspectors also reviewed the TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
SACS heat exchanger relief valve maintenance due to a missed past operability evaluation on October 14 5023 New Freedom offsite line planned maintenance on October 22 00-K-107 Service Air compressor unplanned maintenance following a trip on November 16 SSW pump and HPCI planned maintenance on December 3
b. Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments
a. Inspection Scope
The inspectors reviewed operability determinations for the following degraded or non-conforming conditions based on the risk significance of the associated components and systems: (RHR) flow transmitter equalizing valve mis-positioning on August 31 Review of the SBO calculations as a result of NOTF 20702550 on September 14 Review of the SACS heat exchanger relief valve maintenance due to a missed past operability evaluation on October 14 Review of the overdue environmental qualification preventive maintenance for six conduit seals housing HPCI and RCIC temperature switches on December 11 The inspectors evaluated the technical adequacy of the operability determinations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TSs components or systems were operable. The inspectors confirmed, where appropriate, compliance with bounding limitations associated with the evaluations. Where compensatory measures were required to maintain operability, such as in the case of operator workarounds (OWAs), the inspectors determined whether the measures in place would function as intended and were properly controlled by PSEG. Based on the review of the selected OWAs listed above, the inspectors verified that PSEG identified OWAs at an appropriate threshold and addressed them in a manner that effectively managed OWA-related adverse effects on operators and SSCs.
b. Findings
Introduction:
The inspectors identified a finding because PSEG did not follow procedures to ensure that an identified CAQ was adequately evaluated, documented, and corrected. Specifically, PSEG identified a CAQ associated with an SBO design calculation used to justify the MCR heat load during a loss of ventilation, but failed to adequately evaluate, document and correct the CAQ. This CAQ challenged the reasonable assurance of functionality of the MCR during an SBO event and required PSEG to complete a detailed TE to prove functionality was maintained.
Description:
An SBO event assumes that the initiating event is a loss of offsite power to the site. All sites are required to have procedures and equipment to ensure the satisfactory performance of necessary decay heat removal systems are maintained for the required Sto cope with a four hour SBO, with subsequent restoration of offsite power, with the reactor core remaining covered. PSEG design calculation, H-1-GK-MDC-0735, Electrical Heat Load during an SBO Event (CALC-0735), calculated the amount of heat dissipated by electrical equipment in dominant areas of concern (DACs) during an SBO event. HC.DE-PS.ZZ-0041, Hope Creek SBO Program, Section 5.2.7, Hope Creek SBO Effects of Loss of Ventilation, states that equipment located in DAC condition 1 rooms are considered to be of low concern with respect to elevated temperature effects and will likely require no specific actions to assure functionality for a four hour SBO. Condition 1 is defined by a steady-state temperature of 120 degrees Fahrenheit. PSEG defines the MCR (Room 5110) as a condition 1 room and states that NUMARC 87-00, Section 2.7.2 assures functionality of equipment in condition 1 rooms if the room temperature is less than or equal to 120 degrees Fahrenheit. The electrical heat loads from CALC-0735 are the design input for PSEG design calculation, H-1-GK-MDC-0734, Loss of Ventilation during SBO (CALC-0734), which determines the maximum steady state room air temperatures in the DACs, that includes the MCR. During a daily review of NOTFs conducted on September 14, the inspectors noted that NOTF 20702550 documented calculation error in CALC-0735. This error involved an unaccounted electrical load of 2,520 watts that was incorrectly not included in the MCR heat load total (22,778.7 watts).
Prior to the identification of the error, CALC-0734 determined the maximum steady state MCR temperature to be 118.8 degrees Fahrenheit. This calculated value was less than 120 degrees Fahrenheit that assures functionality of the SBO equipment located in the DACs per NUMARC 87-00, Section 2.7.2 guidance. The inspectors observed that PSEG operators screened NOTF 20702550 on September 14 as an operable but degraded or non-conforming condition requiring an operability evaluation (OPEVAL) or TE. NOTF 20701091 was created for the performance of the OPEVAL. The inspectors found that operations re-screened the issue on September 17, 2015, as functional plant conditions. On September 17, 2015, engineering also reviewed the NOTF and considered the issue a CC-AA-11 non-conformance as deficiency in characteristic, documentation, or procedure that renders the quality of a SSC or activity unacceptable or indeterminate. Therefore the inspectors considered this issue a CAQ in accordance with LS-AA-120 Section 2.2 that defines a CAQ, in part, as deficiencies and non-conformances associated with SSCs and conditions that impact regulated events such as SBO. The (MRC) and Station Ownership Committee (SOC) had both reviewed the initial NOTF, cancelled the assigned OPEVAL, and failed to create an action to perform the required evaluation of the non-conforming condition or an action to review functionality of the MCR during an SBO event. On September 25, 2015, the inspectors met with PSEG regulatory assurance and engineering personnel to discuss the non-conforming condition and questioned why no evaluation or review of past operability of the issue had been performed per PSEG procedure, OP-AA-108-115, Operability Determinations and Functionality Assessments. Due to the inspectors questions, PSEG initiated NOTF 20704285 documenting the to SOC, citing the need for a documented basis for current and past operability and initiated a TE (70180302). On October 19, 2015, PSEG engineering recognized additional errors in CALC-0735, and calculated the revised MCR heat load total as 25,298.7 watts. TE (70180302), completed on October 22, 2015, 38 days after the CAQ was identified, determined that using the revised heat load of 25,298.7 watts, which included the unaccounted for electrical load of 2,520 watts, in CALC-0734 yielded a maximum steady-state temperature of 122.4 degrees Fahrenheit in the MCR. This result being above 120 degrees Fahrenheit validated the initial CAQ and the potential to impact the functionality of the MCR during an SBO event. realistic pre-event temperaturesconservative initial temperatures than were previously used with the design basis calculations) for the MCR and surrounding areas to acquire additional margin in the design calculation. These temperatures were taken by PSEG from other design calculations used for the MCR cooling and ventilation design. Utilizing these temperatures as an input to CALC-0734, PSEG determined that the real MCR temperature would only get as high as 116 degrees Fahrenheit, or 4 degrees below the maximum acceptable room temperature to assure current functionality.
As noted previously, PSEG procedure, LS-AA-120, Issue Identification and Screening Process, Section 2.2 defines CAQ as, in part, as deficiencies and non-conformances associated with SSCs and conditions that impact regulated events such as SBO. The inspectors determined that PSEG failed to adequately evaluate, document, and correct the identified CAQ until the ievaluation of the issue. ded performing a detailed TE to ensure MCR temperatures during an SBO would not have exceeded a functionality limit, and initiating actions to ensure issues identified a potential CAQ get the appropriate screening by operators, engineering and management staff. PSEG also revised SBO procedures to ensure the proper electrical loads were included when required to be shed in the event of an SBO event. PSEG documented the issue in the CAP as NOTF 20704285.
Analysis.
The failure to follow PSEG procedures, LS-AA-120 and OP-AA-108-115, to adequately evaluate, document, and correct a CAQ associated with an SBO design calculation used to justify main control room MCR heat load during a loss of ventilation was a performance deficiency that was reasonably within Pcorrect and which should have been prevented. The issue was evaluated in accordance with IMC 0612, Appendix B, and determined to be more than minor, and therefore a finding, since it was associated with the human performance attribute of the Mitigating Systems cornerstone and adversely affected its objective to ensure capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the calculation error resulted in the main control room temperatures exceeding the functionality temperature limit of the installed equipment until additional calculations could be completed. Additionally, the finding was similar to IMC 0612, Appendix E, examples j and k, in that, a design engineering calculation error resulted in a condition where there was a reasonable doubt of functionality of an SSC. The finding was Determination Process (SDP) for Findings-at-screened as very low safety significance (Green) using Exhibit 2 for Mitigating Systems Screening Questions, because the finding is a deficiency affecting the design or qualification of a mitigating SSC, but the affected SSC maintains its operability and/or functionality. Specifically, the design calculation error was a CAQ that challenged the reasonable assurance of operability of the MCR during an SBO event and required a TE to prove functionality of the MCR during an SBO event was maintained.
The inspectors determined this finding has a cross-cutting aspect in the area of PI&R, Evaluation, in that PSEG did not thoroughly evaluate the issue to ensure that resolutions address causes and extent of conditions, commensurate with its safety significance. Specifically, PSEG did not ensure that this issue of concern was properly classified, prioritized, and evaluated according to its safety significance, and operability and reportability determinations were not developed, when appropriate. (P.2)
Enforcement:
SBO analysis for the MCR in not safety-related and no violation of regulatory requirements occurred. PSEG documented the issue in the CAP as NOTF 20704285. Because this finding does not involve a violation and has very low safety significance, it is identified as a finding. (FlN 05000354/2015004-01, Failure to Follow CAP Procedures to Ensure Functionality of the Main Control Room during a Station Blackout)
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed the post-maintenance tests for the maintenance activities listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions.
Filtration, recirculation, and ventilation system vent RMS flow control loop malfunction on October 15 (Order 60126154) SSW pump and motor replacement on October 24 (Orders 30104990 and 30137509), pump minimum flow check valve following valve disassembly on November 20 (Order 60127049) 00-K-107 service air compressor reassembly and testing on December 5 (Order 30259246)
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR, and PSEG procedure requirements. The inspectors verified that test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied. Upon test completion, the inspectors considered whether the test results supported that equipment was capable of performing the required safety functions. The inspectors reviewed the following surveillance tests: HC.OP-ST.KJ- HC.OP-IS.EG- HC.OP-IS.BC-0102, on November 14
b. Findings
No findings were identified.
Cornerstone:
1EP6 Drill Evaluation
Emergency Preparedness Drill Observation
a. Inspection Scope
The inspectors evaluated the conduct of a routine PSEG emergency drill on December 15 to identify any weaknesses and deficiencies in the classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the simulator, technical support center, and emergency operations facility to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the drill critique to compare inspector observations with those identified by PSEG staff in order to identifying weaknesses and entering them into the CAP.
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstones: Occupational and Public Radiation Safety
2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation
a. Inspection Scope
The inspectors verified the effectiveness of PSEG programs for processing, handling, storage, and transportation of radioactive material. The inspectors used the requirements of 49 CFR 170 through 177; 10 CFR 20, 37, 61, and 71; applicable industry standards; regulatory guides, and procedures required by TSs as criteria for determining compliance.
Inspection Planning
The inspectors conducted an in-office review of the solid radioactive waste system description in the UFSAR, the process control program (PCP), and the recent radiological effluent release report for information on the types, amounts, and processing of radioactive waste disposed. The inspectors reviewed the scope of quality assurance (QA) audits performed for this area since the last inspection.
Radioactive Material Storage The inspectors observed radioactive waste container storage areas and verified that PSEG Hope Creek had established a process for monitoring the impact of long-term storage of the waste. Radioactive Waste System Walk-down The inspectors walked down the following items and areas: Accessible portions of liquid and solid radioactive waste processing systems to verify current system alignment and material condition Abandoned in place radioactive waste processing equipment to review the controls in place to ensure protection of personnel Changes made to the radioactive waste processing systems since the last inspection Processes for transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers Current methods and procedures for dewatering waste Waste Characterization and Classification The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.
Shipment Preparation The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and licensee verification of shipment readiness. Shipping Records The inspectors reviewed selected non-excepted package shipment records. Identification and Resolution of Problems The inspectors assessed whether problems associated with radioactive waste processing, handling, storage, and transportation, were identified at an appropriate threshold and properly addressed in PSEG CAP.
b. Findings
One finding was identified by the licensee, as described in Section 4OA7.
OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification
.1 Safety System Functional Failures
a. Inspection Scope
PI for Hope Creek for the period of January 1, 2015, through December 31, 2015. To determine the accuracy of the PI data reported during those periods, inspectors used definitions and guidance contained in Nuclear Energy Institute (NEI) Document 99-02, -rule records, maintenance WOs, condition reports, event reports and NRC integrated inspection reports to validate the accuracy of the submittals.
b. Findings
No findings were identified.
.2 Occupational Exposure Control Effectiveness
a. Inspection Scope
During the weeks of November 2, and December 14, 2015, the inspectors sampled PSEG submittals for the occupational radiological occurrences PI for the fourth quarter 2014 through the third quarter 2015. The inspectors used PI definitions and guidance contained in the NEI Document 99-02, Revision 7, to determine the accuracy of the PI radiation safety to determine if the related data was adequately assessed and reported. The inspector reviewed electronic personal dosimetry accumulated dose alarms, dose reports, and dose assignments for any intakes that occurred during the time period reviewed to determine if there were any unreported PI occurrences. The inspectors also conducted walk-downs of various locked high and very high radiation area entrances to determine the adequacy of the controls in place for these areas.
b. Findings
No Findings were identified.
.3 Radiological Effluent TS/ODCM Radiological Effluent Occurrences
a. Inspection Scope
During the weeks of November 2 and December 14, 2015, the inspectors sampled PSEG submittals for the radiological effluent TS/ODCM radiological effluent occurrences PI for the fourth quarter 2014 through the third quarter 2015. The inspectors used PI definitions and guidance contained in the NEI Document 99-02, Revision 7, to determine if the PI data was reported properly. The inspectors reviewed the public dose assessments (gaseous and liquid) for the PI for public radiation safety to determine if related data was accurately calculated and reported. The insgenerated since this indicator was last reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose. The inspectors reviewed gaseous and liquid effluent summary data and the results of associated offsite dose calculations to determine if indicator results were accurately reported. Included in this review were PSEG calculations and public dose projections associated with effluent releases from the Turbine Building Roof Turbine Lube Oil vents.
b. Findings
No Findings were identified.
4OA2 Problem Identification and Resolution
.1 Routine Review of Problem Identification and Resolution Activities
a. Inspection Scope
the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that PSEG entered issues into the CAP at an appropriate threshold, gave adequate attention to timely corrective actions, and identified and addressed adverse trends. In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP and periodically attended condition report screening meetings. The inspectors also confirmed, on a sampling basis, that, as applicable, for identified defects and non-conformances, PSEG performed an evaluation in accordance with 10 CFR Part 21.
b. Findings
No findings were identified.
.2 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a semi-annual review of site issues, as required by Inspection indicate the existence of more significant safety issues. In this review, the inspectors included repetitive or closely-related issues that may have been documented by PSEG outside of the CAP, such as trend reports, PIs, department and station performance improvement integrated matrices, system health reports, maintenance rule assessments, and maintenance or CAP backlogs. The inspection also reviewed CAP database for the third and fourth quarters of 2015 to assess the condition report review (Section 4OA2.1).
b. Findings and Observations
No findings were identified. The inspectors determined that any performance deficiencies associated with the trends discussed below were either captured in previous findings (as noted below), or were of minor significance in accordance with IMC 0612, Appendix B.
Maintenance Rule Program Implementation impact of an equipment issue on interfacing systems, including: In September 2013, the inspectors identified that PSEG failed to evaluate the impact of a failure of a feedwater crosstie valve on the feedwater sealing functions for the reactor core isolation cooling system and HPCI system. This observation resulted in the creation of a new feedwater system maintenance rule function and subsequent maintenance preventable functional failure classification that would not have been otherwise counted. (NOTF 20619913) In May 2014, the inspectors identified that PSEG failed to evaluate safety relief valve setpoint failures under all applicable interfacing system functions. The condition was evaluated for the automatic depressurization system functions, but not for the main steam functions. (NOTF 20650346) In August 2015, the inspectors identified that PSEG failed to evaluate the loss of the 10B431 480VAC (alternating current) 1E motor control center (MCC) as a Maintenance Rule functional failure of the interfacing 1E 480VAC system. This is the third instance identified in three years of PSEG failing to evaluate the impact of equipment issues on interfacing systems. This observation resulted in the assignment of a maintenance preventable functional failure to the 480VAC 1E MCC system that would not have been otherwise counted. (NOTF 20702217) Along with the items described above, during 2015, the inspectors and the NRC PI&R team inspectors observed multiple other impact of an equipment issue on interfacing systems. These repetitive observations related to interfacing system maintenance rule screening resulted in PSEG creating a maintenance rule panel consisting of the maintenance rule program coordinator and engineers that performs an independent, periodic review of issues identified in the CAP to ensure all appropriate screenings are assigned. The inspectors determined that the corrective action implemented to address the issue was reasonable to resolve the identified deficiencies. The inspectors determined all the issues above screened to minor in accordance with IMC 0612, Appendix E, because the system equipment performance as provided in paragraph (a)(2) of the maintenance rule. Locked High Radiation Area (LHRA) Controls In the semi-annual trend in Section 4OA2.2 of the second quarter 2015 Hope Creek inspection report (IR 05000354/2015002), the inspectors documented a review of multiple instances of improperly secured LHRA doors. Subsequently, the inspectors documented a Green NCV in the third quarter 2015 Hope Creek inspection report (NCV 05000354/2015003-02) when a worker did not comply with a radiological barrier and posting, and entered a LHRA without proper authorization.
The inspectors reviewed a focused area self-assessment initiated to evaluate the LHRA control events (Order 70175974). The inspectors performed a review of the design change installed as a corrective action to address the equipment issues that resulted in improperly secured LHRA doors. The design change installed an alternate locking mechanism to address degraded door locks for LHRA doors. The inspectors performed walkdowns and challenged the LHRA barriers that have had the new alternate locking mechanisms installed. The inspectors reviewed and checked the storage and control measures in place for the alternate locking mechanisms that are maintained by the Radiation Protection department. The inspectors determined that the corrective actions implemented to address the issue were reasonable to resolve the identified deficiencies.
.3 Annual Follow-up Sample: Masterpact 480 Volt Circuit Breaker Trips
a. Inspection Scope
The inspectors performed an in- and resolution regarding numerous sporadic trips of 480 volt safety-related Masterpact circuit breakers. Specifically, Hope Creek experienced 25 sporadic breaker trips immediately following breaker closure since the Masterpact breakers were installed in plant switchgear in 2004 as replacements for obsolete breakers. The Masterpact circuit breakers uses a micrologic trip unit to provide protection. The trip unit monitors breaker parameters and trips the breaker on overcurrent (short time and long time) and ground fault. The micrologic trip units also contain an internal advanced protection (AP) feature to protect the breaker and associated load in the event of a trip unit failure. For most of the sporadic trips following breaker closure events, the micrologic unit indicated the trip feature (overcurrent, ground fault, or AP that caused the breaker to trip. There were five trips that occurred and no trip feature was indicated. For all of these events, no abnormalities were found with the associated circuit. Following a failure on February 25, 2015, PSEG initiated an apparent cause evaluation (ACE) to determine the cause of the sporadic trips. The inspectors performed an in-depth review of ACE and corrective actions associated with the issue documented in Order 70174219.
The inspectors assessed PSEGextent of condition reviews, and the prioritization and timeliness of corrective actions to determine whether PSEG was appropriately identifying, characterizing, and correcting problems associated with these issues and whether the planned or completed corrective actions were appropriate. The inspectors compared the actions taken to the CAP and 10 CFR 50, Appendix B. In addition, the inspectors reviewed documentation associated with this issue, interviewed engineering and maintenance personnel, and information related to testing performed by outside vendors.
b. Findings and Observations
No findings of significance were identified.
To determine the cause of the sporadic trips, PSEG assembled a complex troubleshooting team to analyze the failures. Twelve potential causes were identified. The majority of the potential causes were either ruled out or partially ruled out by the complex troubleshooting. The ACE concluded that the most probable cause was excessive electro-magnetic interference (EMI) in the vicinity of the circuit breakers. PSEG came to this conclusion because 17 of the spurious trips occurred within the same two circuit breaker cubicles locations on all eight Class 1E 480 volt unit substations. The circuit breaker cubicles are physically located in close proximity to 4kV/480V transformers and the affected circuit breakers power induction motors with large starting currents. Based on this, the inspector most probable apparent cause of sporadic breaker trips being excessive EMI orrective actions included working with an outside vendor and the circuit breaker supplier to perform an in-plant EMI survey to confirm that excessive EMI occurs during breaker closure at the breaker cubicles involved and to develop repairs or modifications to protect against the EMI.
In April 2015, PSEG received the results of the in-plant EMI survey from an outside vendor. The report concluded that the EMI profile in the area of the breaker cubicles associated with sporadic circuit breaker trips was elevated upon circuit breaker closure, however, the levels did not exceed the levels which the circuit breakers were qualified to. The outside vendor recommended that additional transient testing of the breakers and micrologic trip units be performed under full load and during dynamic conditions including breaker closure. Additional testing was performed by the circuit breaker supplier on circuit breakers and micrologic trip units which had experienced sporadic trips. However, no sporadic trips could be recreated during the testing.
Based on the results of the testing, PSEG revisited complex troubleshooting of the problem. All possible failure mechanisms were refuted with the exception of a possible flaw in the digital software of the Masterpact micrologic trip units. At the time of the inspection, PSEG was planning on having an outside vendor perform an independent validation of the complex troubleshooting that PSEG completed to verify that there were no other potential failure mechanisms. PSEG then planned to perform a review of the micrologic trip unit software.
The inspectors noted that the original due date for completing corrective actions was June 19, 2015. At the time of the inspection, the due date, which had been extended four times, was January 19, 2016. Due to the complexity of problem, PSEG has had to work with outside vendors which has contributed to the delays in implementing corrective actions. However, the inspectors concluded that PSEG could have taken actions to address other potential causes other than EMI (i.e., potential micrologic software flaw) in parallel with additional testing following the discovery that the EMI levels at the effected breaker cubicles did not exceed the levels that the circuit breakers were qualified to. Order 70174319 contained an action item to revise the apparent cause if testing, the EMI survey, or vendor recommended actions determined that EMI was not the cause of the breaker trips. However, the inspectors noted that there were no items in the CAP to schedule or track actions to further investigate the potential digital software flaw. The inspectors noted that Operations was tracking the issue on the Operations Concerns List which appeared to be driving the actions to address the potential flaw. PSEG entered the issue into the CAP as NOTF 20711720 to formally track, direct actions, and to initiate corrective actions within the CAP as a result . Based on the information described above, the inspectors did not identify any findings of significance. However, the inspectors briefed PSEG on two observations: 1) corrective actions were not timely and could have pursued other potential causes in parallel; and, 2) to further investigate the identified potential digital software flaw with the breakers. While neither of these observations were determined to be more than minor by the inspectors, PSEG entered the
.4 Annual Follow-up Sample: Review of Root Cause Evaluation Procedure Implementation
a. Inspection Scope
The inspectors performed an in-depth review of root cause evaluations for a loss of shutdown cooling that occurred on April 11, 2015 (70175589), and a redundant reactivity control system (RRCS) automatic actuation that resulted in a reactor scram on September 28, 2015 (70180315). This review by the inspectors was the direct result of observations made during the recent NRC PI&R team inspection conducted in February 2015 (See IR 05000354/2015008).
extent of condition reviews, compensatory actions, and the prioritization and timeliness of PSEG's corrective actions to determine whether PSEG was appropriately identifying, characterizing, and correcting problems associated with these two issues and whether the planned or completed corrective actions were appropriate. The inspectors compared the actions taken to the requirements of PSEG's CAP and 10 CFR 50, Appendix B,
b. Findings and Observations
No findings were identified. The inspectors reviewed previous observations made by the NRC PI&R team in February 2015, that three out of six RCEs over the last two years had problems with the implementation of the RCE procedure, the implementation of corrective actions, and the ability of PSEG to follow through on corrective actions taken to prevent the reoccurrence of significant conditions adverse to quality. Along with the information reviewed above, RCE Manual, LS-AA-125-1001, to ensure PSEG was following the established processes in their procedure for a consistent outcome. The inspectors observed station challenge meetings and MRC review meetings to the RCE conclusions and accurately assign corrective actions to the root and contributing causes. The inspectors noted that who effectively challenged the quality of the reviewed RCE products. The inspectors also noted that PSEG appropriately diversified each of the RCE teams, utilizing a multidisciplinary team to conduct the RCEs.
For both RCEs performed, the inspectors concluded that PSEG appropriately implemented the RCE procedure and addressed the root and contributing causes with appropriate corrective actions.
4OA3 Follow-Up of Events and Notices of Enforcement Discretion
Plant Events
a. Inspection Scope
For the plant events listed below, the inspectors reviewed and/or observed plant parameters, reviewed personnel performance, and evaluated performance of mitigating systems. The inspectors communicated the plant events to appropriate regional personnel, and cactivities. As applicable, the inspectors verified that PSEG made appropriate emergency classification assessments and properly reported the event in accordance with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed follow-up actions related to the events to assure that PSEG implemented appropriate corrective actions commensurate with their safety significance.
An unplanned automatic reactor scram on September 28, 2015
b. Findings
No findings were identified.
4OA6 Meetings, including Exit
On January 16, 2016, the inspectors presented the inspection results to Mr. P. Davison, Site Vice President, and other members of the Hope Creek staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report. PSEG management acknowledged and did not dispute the findings.
4OA7 Licensee-Identified Violations
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as a non-cited violation: From 2010 to 2014, Hope Creek made a total of 12 shipments of radioactive waste for disposal, four of which contained a category 1 quantity of radioactive material, and eight which contained a category 2 quantity of radioactive material of concern. PSEG did not implement a transportation security plan for these This performance deficiency adversely affected the Public Radiation Safety cornerstone attribute of Program and Process based on inadequate procedures associated with the transportation of radioactive material. The finding was determined to be of very low safety significance (Green) because Hope Creek had an issue involving transportation of radioactive material, but it did not involve: (1) a radiation limit that was exceeded; (2) a breach of package during transport; (3) a certificate of compliance issue; (4) a low level burial ground non-conformance; or (5) a failure to make notifications or provide emergency NOTF 20674767. Corrective actions included issuance of new procedure RP-AA-600-1009, revision of procedure LS-AA-notifications of potentially applicable rule changes in the Federal Register.
ATTACHMENT:
SUPPLEMENTARY INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- P. Davison, Site Vice President
- E. Carr, Plant Manager
- D. Bartlett, Engineering Branch Manager Electrical and Instrumentation and Controls
- P. Bellard, IST Program Engineer
- H. Berrick, Regulatory Assurance Learning Programs Specialist
- M. Biggs, Maintenance Rule Program Coordinator
- A. Contino, System Engineer
- S. Dennis, Hope Creek Operations Training
- G. Klekos, Radioactive Materials Shipper
- P. Koppel, Maintenance Engineer
- T. MacEwen, Regulatory Assurance
- J. Priest, Nuclear Shift Operations Manager
- P. Quick, Emergency Preparedness Program Manager
- L. Sinclair, Emergency Preparedness Technical Specialist
- J. Thompson, Procurement Engineer
- K. Thompson, Radiological Engineer
- K. Timko, System Engineer
- H. Trimble, Radiation Protection Manager
LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED
Opened/Closed
- 05000354/2015004-01 FIN Failure to Follow CAP Procedures to Ensure Functionality of the Main Control Room during a Station Blackout (Section 1R15)
LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
Procedures
- HC.OP-AB.MISC-0001, Acts of Nature, Revision 28
- OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 13
Notifications
- 20689082
Section 1R04: Equipment Alignment
Procedures
- HC.OP-SO.EA-0001, Service Water System Operation, Revision 39
- HC.OP-ST.BD-0001, RCIC Piping and Flow Path Verification
- Monthly, Revision 14
- HC.OP-ST.EA-0001, Service Water Flow Path Verification
- Monthly, Revision 11
- HC.OP-ST.SV-0001, Remote Shutdown Monitoring Instrumentation Channel Check
- Monthly, Revision 26
Notifications
- 20706937
Drawings
- C-0931-0, Containment Vessel Requirements Suppression Chamber Penetrations Plans, Sections & Details, Revision 18 J-J1301-- M-10-1, Sheet 1, Service Water, Revision 55 M-10-1, Sheet 2, Service Water, Revision 44 M-49-1, Sheet 1, Reactor Core Isolation Cooling, Revision 18 M-50-1, Sheet 1, RCIC Pump Turbine, Revision 19
Section 1R05: Fire Protection
Procedures
- ER-AA-2002, System Health Indicator Program, Revision 14
- ER-AA-2030, Conduct of Plant Engineering Manual, Revision 12
- FP-AA-015, Compensatory Measure Firewatch Program, Revision 6
- FP-HC-004, Actions for Inoperable Fire Protection
- Hope Creek Station, Revision 3
- FRH-II-531, Hope Creek Pre Fire Plan Diesel Generator Rooms, Revision 8
- FRH-III-141, Hope Creek Pre-Air Equipment Area), Revision 4
- HC.OP-AB.COMP-00001, Instrument and/or Service Air, Revision 7
- LS-AA-120, Issue Identification and Screening Process, Revision 13
- LS-AA-125, Corrective Action Program, Revision 21
- MA-AA-716-230, Predictive Maintenance Program, Revision 8
- MA-AA-716-230-1001, Oil Analysis Interpretation Guideline, Revision 11
- MA-AA-716-230-1010, Fluid Leak Management Program, Revision 3
- OP-AA-102-102, General Area Checks and Operator Field Rounds, Revision 8
- OP-AA-108-111, Adverse Contingency Monitoring and Contingency Planning, Revision 11
- WC-AA-106, Work Screening and Processing, Revision 17
Notifications
(*NRC-identified)
- 20670595
- 20676716
- 20690665
- 20701189
- 20702555
- 20705323
- 20705525
- 20706887
- 20707835
- 20710548
- 20712663
- 20712672
- 20712674
- 20712690
- 20712729
- 20710293*
- Maintenance Orders/Work Orders
- 30186636
- 30197172
- 30197310
- 30259173
- 30259246
- 30264931
- 70172400
- 70174237
- 70182267
Miscellaneous
- H-C-KC-MSE-0825, 10CFR50.59 Review and Safety Evaluation
- Use of Salem Fire Suppression Water System as a Backup to Hope Creek, Revision 0 S-C-FP-MSE-0824, 10CFR50.59 Review and Safety Evaluation
- Use of Hope Creek Fire Suppression Water System as a Backup to Salem, Revision 0
Section 1R06: Flood Protection Measures
Drawings
- M-5003, Fire - M-97-0, Bldg. & Equip. Drains
- Aux. Bldg. Control & Diesel Areas Oily, Normal & Chemical Waste Systems, Revision 16 P-2703-- P-2803--
Miscellaneous
- Calculation Number 19-0018, Max. Flood Levels in Control/DG Areas, Revision 8
- HC-PRA-012, Internal Flood Evaluation Summary and Notebook, Revision 2
- HC-PRA-017, Internal Flood Walkdown Notebook, Revision 0
Section 1R11: Licensed Operator Requalification Program
Procedures
- HC.MD-PM.ZZ-0010, Control Panel Preventive Maintenance, Revision 15
- HC.OP-AB.ZZ-0003, Reactor Scram, Revision 3
- HC.OP-IO.ZZ-0003, Startup from Cold Shutdown to Rated Power, Revision 108
- MA-AA-716-012, Post Maintenance Testing, Revision 20
- MA-AA-716-232-1004, Failure Analysis Tracking and Reporting, Revision 2
- TQ-AA-106-0305, Licensed Operator Requalification Training Examination Administration Job Aid, Revision 5
Notifications
- 20711484
- 20497914
- 20698801
- 20704488
- Maintenance Orders/Work Orders
- 30233455
- 60097601
- 60125943
- 70083956
- 70180697
- 80115116
Other Documents
- ESG-074, RWCU Pump Trip/SACS Pump Trip/LOCA/ATWS/CRD FCV Failure/HPCI Start Failure, Revision 12 Hope Creek Maintenance Plan
- 172818 Hope Creek Narrative Logs dated September 30 through October 2, 2015 PCM Template for Low Voltage Circuit Breakers, Revision 3
- PN1-B31-1030-0024, Sht. 11 & 20
- PN1-B31-P003-0215, Sht. 4
- PSE-25953, Failure Analysis of a Protective Relay / Fuses dated 28 December 2015
Section 1R12: Maintenance Effectiveness
Procedures
- EP-HC-111-103, Section R
- Abnormal Rad Levels/Rad Effluent, Revision 0
- EP-HC-111-130, Hope Creek Event Classification Guide Wall Chart (All Modes), Revision 1
- ER-AA-310-1001, Maintenance Rule
- Scoping, Revision 6
- ER-AA-310-1001-F1, Maintenance Rule Scoping Change Request Form, Revision 0
- ER-HC-310-1009, Hope Creek Generating Station Maintenance Rule Scoping, Revision 11
- HC.EP-EP.ZZ-0301, Shift Radiation Protection Technician Response, Revision 8
- HC.OP-EO.ZZ-103/4-CONV, Secondary Containment Control Conversion, Revision 7
- HC.OP-EO.ZZ-103/4-FC, Secondary Containment Control, Revision 10
Notifications
(*NRC identified)
- 20639414
- 20654858
- 20663066
- 20693100
- 20694030
- 20695651
- 20699246
- 20704699
- 20706724
- 20709560
- 20710917
- 20711743
- 20712694
- 20714332
- 20711929*
- 20714121*
- Maintenance Orders/Work Orders
- 60125228 70182741
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Procedures
- ER-AA-2002, System Health Indicator Program, Revision 14
- ER-AA-2030, Conduct of Plant Engineering Manual, Revision 12
- ER-HC-321-1011, Testing of Hope Creek ASME Class 1, 2, 3 Safety Relief Valves, Revision 4
- FRH-III-141, Hope Creek Pre-Air Equipment Area), Revision 4
- HC.MD-GP.ZZ-0085, Safety/Relief Valve Leak Testing and Setpoint Adjustments, Revision 12
- HC.OP-AB.BOP-0004, Grid Disturbances, Revision 24
- HC.OP-AB.COMP-00001, Instrument and/or Service Air, Revision 7
- HC.OP-AB.COOL-0001, Station Service Water, Revision 21
- HC.OP-AB.COOL-0002, Safety/Turbine Auxiliaries Cooling System, Revision 8
- HC.OP-AR.MH-0004, Switchyard Control House Local Panel
- XA-12, Revision 4
- HC.OP-IS.BJ-0001, HPCI Main and Booster Pump Set
- 0P204 and 0P217
- Inservice Test, Revision 64
- HC.OP-SO.EA-0001, Service Water System Operation, Revision 39
- HC.OP-SO.EG-0001 Safety and Turbine Auxiliaries Cooling Water System, Revision 54
- LS-AA-120, Issue Identification and Screening Process, Revision 13
- LS-AA-125, Corrective Action Program, Revision 21
- MA-AA-716-230, Predictive Maintenance Program, Revision 8
- MA-AA-716-230-1001, Oil Analysis Interpretation Guideline, Revision 11
- MA-AA-716-230-1010, Fluid Leak Management Program, Revision 3
- OP-AA-102-102, General Area Checks and Operator Field Rounds, Revision 8
- OP-AA-108-111, Adverse Contingency Monitoring and Contingency Planning, Revision 11
- OP-AA-108-115, Operability Determinations & Functionality Assessments, Revision 4
- WC-AA-106, Work Screening and Processing, Revision 17
Notifications
- 20670595
- 20676716
- 20681254
- 20685208
- 20686020
- 20690665
- 20691433
- 20701189
- 20702555
- 20705472
- 20705653
- 20706118
- 20707034
- 20707835
- 20709840
- 20710548
- 20712199
- 20712211
- 20712663
- 20712672
- 20712674
- 20712690
- 20712729
- Maintenance Orders/Work Orders
- 30115803
- 3025917
- 30259246
- 30278309
- 50177227
- 50179391
- 50180060
- 60117364
- 70115816
- 70142153
- 70172400
- 70174237
- 70174553
- 70175648
- 70177231
- 70179753
- 70182267
Miscellaneous
- Calculation
- EA-0001, Station Service Water System Hydraulic Model, Revision 6 Calculation
- EG-0048, Eval of SACS System Capability following Design Basis Earthquake, Revision 2 HCGS PRA Risk Eval Form for November 29, 2015, through December 5, 2015, Revision 0
- VTD 322848, Test Reports for 24 VSN SSWS Pump
- S/N UG04950246-05, Revision 1
Section 1R15: Operability Determinations and Functionality Assessments
Procedures
- CC-AA-11, Nonconforming Materials, Parts, or Components, Revision 5
- ER-AA-310-1004, Maintenance Rule
- Performance Monitoring, Revision 14
- HC.DE-PS.ZZ-0041, Hope Creek Station Blackout Program, Revision 3
- HC.OP-AB.ZZ-0135, Station Blackout / Loss of Offsite Power / Diesel Generator Malfunction, Revision 40
- HC.OP-FT.ZZ-0001, Emergency Area Cooling System (EACS) Room Coolers Functional Test
- 18 Months, Revision 11
- HC.OP-IS.BC-0002, CP202, C Residual Heat Removal Pump In-Service Test, Revision 43
- HC.OP-SO.EA-0001, Service Water System operation, Revision 39
- LS-AA-120, Issue Identification and Screening Process, Revision 13
- OP-AA-108-115, Operability Determinations & Functionality Assessments, Revision 4
Notifications
- 20701377
- 20701395
- 20702550
- 20703642
- 20703941
- 20703948
- 20704285
- 20704447
- 20710683
- 20711033
- 20712812
- 20712849
- Maintenance Orders/Work Orders
- 30123359
- 30177373
- 30214856
- 30238054
- 50177743
- 60124525
- 70180037
- 70180302
- 70180456
- 70180601
- 70182394
- 70182700
Drawings
- Calculation E-6.1, Revision 12 H-1-GK-MDC-0734, Loss of Ventilation during Station Blackout, Revision 3 H-1-GK-MDC-0735, Electrical Heat Load during the Station Blackout Event, Revision 2 M-51-1, Sheet 2, Residual Heat Removal, Revision 43
Miscellaneous
- OP-HC-108-115-1001, Form 1, Technical Specification Action Statement Log,15-262, H1BC-1C-P-Pump, dated September 2, 2015
- OP-HC-108-115-1001, Form 1, Technical Specification Action Statement Log,15-285, B Core Spray Loop, dated September 24, 2015
- OP-HC-108-115-1001, Form 1, Technical Specification Action Statement Log,15-286, H1BC-1B-P-202 H1BC-1D-P-, dated September 24, 2015
- VTD 327173, Qualification Report on United Electric Temperature Switch (B402), Revision 1 VTD PM780AQ-0199, Acton Environmental Test Report, Revision 6
Section 1R19: Post-Maintenance Testing
Procedures
- HC.IC-SC.SP-0002, Process Radiation Monitoring
- Non Divisional Monitor H1SP-1SPRY-4811 Filtration Recirculation Ventilation Sample Flow System, Revision 31
- HC.IC-SC.SP-0025, Process Radiation Monitoring
- Non Divisional Monitor H1SP-1SPRY-4811 Filtration Recirculation Ventilation System Vent (WRGM), Revision 31
- HC.MD-GP.ZZ-0237, General Instructions for Disassembly, Inspection, and Reassembly of Anchor Darling Testable Check Valves, Revision 5
- HC.OP-IS.BC-0003,
- HC.OP-IS.BC-0102,
- Inservice Test,
- Revision 43
- HC.OP-IS.BC-0103, Residual Heat Removal Subsystem C Valves
- Inservice Test, Revision 29
- HC.OP-IS.EA-0002, B Service Water Pump
- BP502
- Inservice Test, Revision 61
- MA-AA-716-008, Foreign Material Exclusion Program, Revision 8
- MA-AA-716-012, Post Maintenance Testing, Revision 20
- MA-AA-734-002, General Instructions for Disassembly, Inspection & Reassembly of Check Valves, Revision 1
Notifications
- 20672012
- 20706227
- 20706724
- 20707029
- 20707289
- 20709447
- 20710441
- 20711033
- 20711671
- Maintenance Orders/Work Orders
- 30104990
- 30123359
- 30137509
- 50165163
- 50176817
- 50177700
- 50178431
- 50179071
- 50179156
- 60124525
- 60126154
- 60126926
- 60127049
- 70041235
- 70172122
- 80077844
- 80081469
Drawings
- M-51-1, P&ID Residual Heat Removal, Revision 47
Section 1R22: Surveillance Testing
Procedures
- HC.MD-GP.ZZ-0237, General Instructions for Disassembly, Inspection, and Reassembly of Anchor Darling Testable Check Valves, Revision 5
- HC.OP-IS.BC-0003, Revision 48
- HC.OP-IS.BC-0102,
- Inservice Test,
- Revision 43
- HC.OP-IS.EG-0001, A SACS Pump
- AP210
- Inservice Test, Revision 40
- HC.OP-ST.KJ-0003, Emergency Diesel Generator 1CG400 Operability Test
- Monthly,
- Revision 76
- MA-AA-716-008, Foreign Material Exclusion Program, Revision 8
- MA-AA-734-002, General Instructions for Disassembly, Inspection & Reassembly of
- Check Valves, Revision 1
Notifications
- 20646523
- 20672012
- 20698460
- 20698577
- 20698606
- 20698941
- 20699027
- 20699521
- 20699989
- 20702217
- 20704921
- 20704923
- 20709447
- 20710441
- Maintenance Orders/Work Orders
- 30123359
- 50174603
- 50176817
- 50177155
- 50178077
- 50178431
- 50179156
- 50179393
- 60126926
- 70041235
- 70165411
- 70172122
- 70179009
- 70179133
- 70179342
- 80077844
- 80081469
Drawings
- M-51-1, P&ID Residual Heat Removal, Revision 47
Section 1EP6: Drill Evaluation
Procedures
- EP-AA-125-1002, NRC Drill and Exercise Performance (DEP) Indicator Guidance, Revision 4
- EP-HC-111-F2, Declaration of Alert, Revision 2
- EP-HC-111-F3, Declaration of Site Area Emergency, Revision 3
- EP-HC-111-F4, Declaration of General Emergency, Revision 2
- EP-HC-111-F6, Primary Communicator Log, Revision 13
- EP-HC-111-F8, Secondary Communicator Log, Revision 3
- NC.EP-EP.ZZ-0404, Protective Action Recommendations (PARS) Upgrades, Revision 5
Notifications
(*NRC-identified)
- 20713379
- 20713545
- 20713846
- 20713863
- 20714656
- 20714758
- 20715510 20714553*
Section 2RS8: Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation
Procedures
- LS-AA-1020, Implementation of Significant Rules and Orders, Revision 1
- RP-AA-100, Process Control Program for Radioactive Wastes, Revision 10
- RP-AA-600, Radioactive Material Waste Shipments, Revision 14
- RP-AA-600-1006, Shipment of Category 1 Quantities of Radioactive Material or Waste (Category 1 RAMQC), Revision 7
- RP-AA-602, Packaging of Radioactive Material Shipments, Revision 16
- RP-AA-602-1001, Packaging of Radioactive Material/Waste Shipments, Revision 9
- RP-AA-605-1001, Evaluation of 10CFR61 Sample Results, Revision 1
- Notifications:
- 20655917
- 20695192
- Audits: Hope Creek Check-In Self-Assessment
- 80114767
- NOSA-HPC-14-04, General Requirements for Shipments Nuclear Utilities Procurement Issues Council Audit 23201, Energy Solutions Mega Audit
- 10CFR61 Scaling Factors: A-CUPS; WSPS; B-Condensate demineralizer Bead Resin; Bead Resin, Dry Active Waste (DAW)
- Training: NRP00MATTSHC, Chem-Nuclear 79-19 NRP9902RMATC, RAM Shipping (79-19)
Section 4OA1: Performance Indicator Verification
Procedures
- LS-AA-2001, Collecting and Reporting of NRC Performance Indicator Data, Revision 11
- LS-AA-2080, Monthly Data Elements for NRC SSFFs, Revision 5
Miscellaneous
- LER 05000354/2015-001-00 and -01, Conditions Prohibited by Technical Specifications Due to Core Spray Inoperabilities dated May 29, and June 30, 2015
- LER 05000354/2015-002-00, Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment dated June 10, 2015
- LER 05000354/2015-003-00, Conditions Prohibited by Technical Specifications Due to Low Pressure ECCS Inoperabilities dated July 6, 2015
- LER 05000354/2015-004-00 and -01, As-Found Values for Safety Relief Valve Lift Set Points Exceed Technical Specification Allowable Limit dated June 30, and August 26, 2015
- LER 05000354/2015-005-00, Reactor Scram due to Invalid RRCS Actuation dated January 5, 2016
Section 4OA2: Problem Identification and Resolution
Procedures
- ER-AA-2002, System Health Indicator Program, Revision 14
- ER-AA-2030, Conduct of Plant Engineering Manual, Revision 12
- ER-AA-310-1004, Maintenance Rule
- Performance Monitoring, Revision 14
- FRH-III-141, Hope Creek Pre-Fire Plan, Turbine Building Air Equipment Area), Revision 4
- HC.MD-CM.PH-0001, 480 Volt MCC Starter Maintenance, Revision 9
- HC.MD-PM.ZZ-0007, Missile Resistant and Watertight Doors P.M., Revision 11
- HC.OP-AB.COMP-00001, Instrument and/or Service Air, Revision 7
- HC.OP-AB.RPV-0009, Shutdown Cooling, Revision 11
- HC.OP-SO.BC-0002, Decay Heat Removal Operation, Revision 33
- HU-AA-1211, Pre-Job Briefings, Revision 12
- LS-AA-115-1003-F2, OPEX Response, Revision 0
- LS-AA-119-1001, Fatigue Management, Revision 4
- LS-AA-120, Issue Identification and Screening Process, Revision 13
- LS-AA-125, Corrective Action Program, Revision 20
- LS-AA-125, Corrective Action Program, Revision 21
- LS-AA-125, Corrective Action Program, Revision 21
- LS-AA-125-1001, Root Cause Evaluation Manual, Revision 9
- LS-AA-125-1005, Coding and Analysis Manual, Revision 7
- MA-AA-716-210-1005, Predefine Change Processing, Revision 6
- MA-AA-716-230, Predictive Maintenance Program, Revision 8
- MA-AA-716-230-1001, Oil Analysis Interpretation Guideline, Revision 11
- MA-AA-716-230-1010, Fluid Leak Management Program, Revision 3
- OP-AA-101-111, Roles and Responsibilities of On-Shift Personnel, Revision 5
- OP-AA-102-102, General Area Checks and Operator Field Rounds, Revision 8
- OP-AA-106-101, Significant Event Reporting, Revision 10
- OP-AA-106-101-1001, Event Response Guidelines, Revision 15
- OP-AA-108-111, Adverse Contingency Monitoring and Contingency Planning, Revision 11
- OU-AA-101-1006, Outage Management Risk and Impact Assessment, Revision 2
- PIA-009, USA Fleet Trending Guide, Revision 3
- SY-AA-102-202, Testing for Cause and Post Event, Revision 17
- WC-AA-106, Work Screening and Processing, Revision 17
Notifications
(*NRC-identified)
- 20624670
- 20640696
- 20666644
- 20670595
- 20676716
- 20679810
- 20680565
- 20682502
- 20682982
- 20683720
- 20684833
- 20684833
- 20684861
- 20684861
- 20684891
- 20685468
- 20686094
- 20686099
- 20686562
- 20689791
- 20690665
- 20693591
- 20694576
- 20695392
- 20695433
- 20696092
- 20696092
- 20696845
- 20698578
- 20698713
- 20699521
- 20701189
- 20701814
- 20702217
- 20702555
- 20703871
- 20703941
- 20704549
- 20704923
- 20705460
- 20707835
- 20710222
- 20710548
- 20710665
- 20710942
- 20711909
- 20712663
- 20712672
- 20712674
- 20712690
- 20712729
- 20714121
- 20711720*
- Maintenance Orders/Work Orders
- 30259173
- 30259246
- 60123177
- 70040435
- 70060872
- 70160516
- 70162269
- 70167500
- 70170527
- 70170535
- 70172037
- 70172037
- 70172400
- 70172811
- 70174237
- 70175889
- 70175974
- 70176141
- 70176937
- 70176937
- 70176937
- 70177017
- 70177017
- 70177880
- 70179133
- 70179342
- 70180096
- 70181428
- 70182192
- 70182267
- 80095620
- 80113526
- 80113526
- 80113996
- 80114188
- 80114279
- 80115148
- 80115315
Miscellaneous
- 10 CFR Part 21 Notification 2005-39-00, Potentially Defective Micrologic Trip Units Nuclear Logistics, Incorporated Root Cause Analysis Report
- RCA-042-351023474-1,
- October 2015 Report Number HOP150401RO-F, Final Report of AMS Testing of Masterpact Breakers with Installed Square D Micrologic Trip Units for Hope Creek Nuclear Generating Station,
- April 2015 Vendor Technical Manual
- 327133, Masterpact NT/NW Universal Power Circuit Breaker,
- PSEG List of Deferred Breaker PMs from 2015 PSEG List of Failed Breakers in 2014 Hope Creek Main Control Room Door Reader Transaction History dated April 11, 2015 October 2003
- Hope Creek Operations Narrative Logs dated April 11, 2015 Hope Creek Narrative Logs from August 3 through August 6, 2015 Hope Creek January
- Sept 2015 Trend Report
- E-0019-1, 480 Volt MCC Tabulation Class 1E
- Aux Building
- O/G Area 10B411, 421,
- 431 and 441 LTAM H-13-0084, MCC Remaining Bucket Replacement dated November 14, 2013