IR 05000220/2008004
Download: ML083101203
Text
November 5, 2008
Mr. Keith Vice President Nine Mile Point Nine Mile Point Nuclear Station, LLC P.O. Box 63 Lycoming, NY 13093
SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000220/2008004 and 05000410/2008004
Dear Mr. Polson:
On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Nine Mile Point Nuclear Station, Units 1 and 2. The enclosed integrated inspection report documents the inspection results discussed on October 24, 2008, with you and members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
This report documents one self-revealing finding and one NRC-identified finding of very low safety significance (Green). One of the findings was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it was entered into your corrective action program (CAP), the NRC is treating this violation as a non-cited violation in accordance with Section VI.A.1 of the NRC's Enforcement Policy. If you contest the non-cited violation noted in this report, you should provide a response with the basis for your denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-001; and the NRC Senior Resident Inspector at Nine Mile Point Nuclear Station.
In accordance with 10 CFR Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/ Glenn T. Dentel, Chief Projects Branch 1 Division of Reactor Projects Docket No.: 50-220, 50-410 License No.: DPR-63, NPF-69
Enclosure:
Inspection Report 05000220/2008004 and 05000410/2008004
w/Attachment:
Supplemental Information cc w/encl:
M. Wallace, Vice - Chairman, Constellation Energy H. Barron, President, CEO & Chief Nuclear Officer, Constellation Energy Nuclear Group C. Fleming, Esquire, Senior Counsel, Nuclear Generation, Constellation Energy Group, LLC M. Wetterhahn, Esquire, Winston & Strawn T. Syrell, Director, Licensing, Nine Mile Point Nuclear Station P. Tonko, President and CEO, New York State Energy Research and Development Authority J. Spath, Program Director, New York State Energy Research and Development Authority P. Eddy, New York State Department of Public Service C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law Supervisor, Town of Scriba P. Church, Oswego County Administator T. Judson, Central NY Citizens Awareness Network D. Katz, Citizens Awareness Network G. Detter, Manager, Nuclear Safety and Security, Constellation Energy
SUMMARY OF FINDINGS
...............................................................................................................3
REPORT DETAILS
..........................................................................................................................5
REACTOR SAFETY
........................................................................................................................5 1R01 Adverse Weather Protection .........................................................................................5
1R04 Equipment Alignment....................................................................................................
.6
1R05 Fire Protection...............................................................................................................
.7 1R06 Flood Protection Measures ...........................................................................................8
1R07 Heat Sink Performance ................................................................................................
.8
1R11 Licensed Operator Requalification Program ................................................................
.8
1R12 Maintenance Effectiveness ..........................................................................................
.9
1R13 Maintenance Risk Assessments and Emergent Work Control ....................................
.9
1R15 Operability Evaluations ...............................................................................................12
1R18 Plant Modifications ......................................................................................................13 1R19 Post Maintenance Testing ..........................................................................................14
1R22 Surveillance Testing ....................................................................................................15 1EP2 Alert and Notification System Testing .........................................................................16
1EP3 Emergency Response Organization Augmentation ....................................................16 1EP4 Emergency Action Level and Emergency Plan Changes ............................................17 1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies ....................17 1EP6 Drill Evaluation
RADIATION SAFETY
....................................................................................................................18 2OS1 Access Control to Radiologically Significant Areas .....................................................18 2OS2 ALARA Planning and Controls ....................................................................................19 2OS3 Radiation Monitoring Instrumentation and Protective Equipment
OTHER ACTIVITIES
......................................................................................................................20
4OA1 Performance Indicator Verification ..............................................................................20
4OA2 Identification and Resolution of Problems ...................................................................21
4OA3 Followup of Events and Notices of Enforcement Discretion .......................................23
4OA5 Other Activities.............................................................................................................26 4OA6 Meetings, including Exit...............................................................................................26 ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
.......................................................................................................A-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
...........................................................A-1
LIST OF DOCUMENTS REVIEWED
...........................................................................................A-2
LIST OF ACRONYMS
..................................................................................................................A-7
- OF [[]]
- FINDIN [[]]
GS
IR 05000220/2008004, 05000410/2008004; 07/01/08 - 09/30/08; Nine Mile Point Nuclear Station,
Units 1 and 2; Maintenance Risk Assessment and Event Followup.
The report covered a three-month period of inspection by resident inspectors and regional
specialist inspectors. One Green non-cited violation (NCV), and one Green finding, were
identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process (SDP)." Findings for which the
NRC's program for overseeing the safe operation of commercial
nuclear power reactors is described in
- NUR [[]]
EG-1649, "Reactor Oversight Process," Revision 4,
dated December 2006.
- A. [[]]
NRC-Identified and Self-Revealing Findings Cornerstone: Initiating Events * Green. A self-revealing finding was identified on July 14, 2008, when inadequate maintenance practices, during replacement and troubleshooting of a Unit 2 radioactive waste sump pump, caused an electrical transient that resulted in the loss of numerous
plant components and required a power reduction. The inadequate maintenance
practices included failure to perform post-maintenance testing and continuation of
troubleshooting despite having obtained results that were not consistent with the
troubleshooting plan. This issue was entered into
- NMP [[]]
NS's corrective action program
for evaluation. The finding was greater than minor because it affected the human performance
attribute of the Initiating Events cornerstone objective to limit the likelihood of those
events that upset plant stability and challenge critical safety functions during shutdown
as well as power operations. The finding was evaluated in accordance with IMC 0609 and determined to be of very low safety significance because the finding did not contribute to both the likelihood of a rector trip and the likelihood that mitigation
equipment or functions would not be available, and did not screen as potentially risk
significant due to external events. The finding had a cross-cutting aspect in the area
of human performance because
- NMP [[]]
NS did not appropriately plan the pump
troubleshooting activity by incorporating abort criteria (H.3.a per
- 10 CFR 50.65(a)(4) was identified for inaccurate risk assessments completed for August 5 and 6, 2008. Specifically, the unavailable reactor core isolation cooling (
RCIC) system was not
properly incorporated into the risk assessment. The cause was determined to be that
an error had been made while entering a change to the risk monitor computer
4software, which resulted in
- RC [[]]
IC incorrectly being assigned a zero risk importance.
As corrective actions, the modeling of
- RC [[]]
IC was corrected and a verification of all
mapping codes used in the risk monitor was performed. The finding was greater than minor because the risk assessment for
- RC [[]]
IC system
maintenance was inadequate due to inaccurate information that was provided to the
risk assessment tool. As a result, the overall elevated plant risk, when correctly assessed, put the plant into a higher licensee-established risk category. The finding
was evaluated in accordance with IMC 0609, Appendix K, and determined to be of
very low safety significance because the incremental core damage probability deficit (ICDPD) was less than 1E-6. The finding had a cross-cutting aspect in the area of human performance because
IMC 0305). (Section 1R13)
- 5REPORT [[]]
DETAILS
Summary of Plant Status
Nine Mile Point Unit 1 began the inspection period at full rated thermal power (RTP). Several
short duration power reductions were performed for maintenance on reactor recirculation pump
(RRP) motor-generators, and on September 27, power was reduced to 68 percent for a control
rod sequence exchange, single rod scram time testing, and turbine valve testing. Power was
restored to 100 percent the following day, and remained there for the rest of the inspection period.
Nine Mile Point Unit 2 began the inspection period at full RTP. On July 14, power was reduced to
percent due to loss of two high pressure feedwater heaters (FWHs), which resulted from an
electrical transient due to an equipment failure. The FWHs were subsequently returned to
service, and power was restored to 100 percent the next day. On September 4, an increase in drywell airborne radioactive particulate activity, along with indication of a slowly degrading pump seal for the 'B' RRP and an apparent rapid increase in drywell unidentified leakage, prompted operators to perform a rapid power reduction to 93 percent. It was later determined that drywell
leakage was actually unchanged and stable, as were 'B' RRP seal parameters. Power was
restored to full RTP later that day. On September 18, power was reduced to 86 percent due to a
problem with the main transformer cooling system. The problem was resolved and power was
restored to full
RTP for the remainder of the
inspection period. 1.
- SAFETY "Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection ([[Inspection procedure" contains a listed "[" character as part of the property label and has therefore been classified as invalid. - One sample) a. Inspection Scope On July 24, 2008, the inspectors reviewed]]
- NMP [[]]
NS's actions in response to a severe
electrical storm in the vicinity of the station. During this storm, Unit 1 experienced a
momentary loss of one of the two 115 kilovolt (kV) offsite power lines (line 1) due to a
lightning strike. Offsite power continued to be supplied to both vital switchboards from
offsite line 4, so this event did not result in an automatic start of the associated emergency
diesel generator (EDG). The affected breaker, onsite supply breaker R-10, automatically
reclosed as designed after approximately 5 seconds. The event did not have any
significant effect on plant operations. The inspectors verified that operators implemented
actions specified in the associated procedure to reduce the impact that the adverse
weather had on the site. The inspectors also verified that the
- NMPNS procedures addressed measures to monitor and maintain availability and reliability of the other offsite alternating current (
AC) power system and the onsite alternate AC power system during adverse weather conditions.
b. Findings
6No findings of significance were identified. 1R04 Equipment Alignment
.1 Partial System Walkdown (71111.04 - Four samples)
a. Inspection Scope The inspectors performed partial system walkdowns to verify risk-significant systems were
properly aligned for operation. The inspectors verified the operability and alignment of
these risk-significant systems while their redundant trains or systems were inoperable or
out of service for maintenance. The inspectors compared system lineups to system operating procedures, system drawings, and the applicable chapters in the updated final
safety analysis report (UFSAR). The inspectors verified the operability of critical system
components by observing component material condition during the system walkdown. The inspectors performed partial walkdowns of the following systems: * Unit 1 core spray system 111 while core spray system 112 was inoperable for in-service testing; * Unit 1 core spray system 12 while the 112 core spray topping pump was inoperable and unavailable for maintenance; * Unit 2 125 volt direct current (DC) electrical system, Divisions 1 and 2, due to high safety significance; and * Unit 2 high pressure core spray (HPCS) system while the reactor core isolation cooling (RCIC) system was inoperable for maintenance. b. Findings No findings of significance were identified.
.2 Complete System Walkdown (71111.04S - One sample)
a. Inspection Scope The inspectors performed a complete walkdown of the Unit 1 emergency service water
(ESW) system to identify discrepancies between the existing equipment configuration and
that specified in the design documents. During the walkdown, system drawings and
operating procedures were used to determine the proper equipment alignment and
operational status. The inspectors reviewed the open maintenance work orders (WOs)
that could affect the ability of the system to perform its functions. Documentation
associated with temporary modifications, operator workarounds, and items tracked by
plant engineering were also reviewed to assess their collective impact on system
operation. In addition, the inspectors reviewed the condition report (CR) database to
verify that equipment alignment problems were being identified and appropriately
resolved.
b. Findings
7No findings of significance were identified. 1R05 Fire Protection
.1 Quarterly Inspection (71111.05Q - Six samples)
a. Inspection Scope The inspectors toured areas important to reactor safety at
- NMP [[]]
NS to evaluate the
station's control of transient combustibles and ignition sources, and to examine the
material condition, operational status, and operational lineup of fire protection systems
including detection, suppression, and fire barriers. The areas inspected included:
- Unit 1 reactor building (RB) 261 foot elevation; * Unit
RB 289 foot elevation; and * Unit 2 RB 353 foot elevation. b. Findings No findings of significance were identified.
.2 Annual Inspection (71111.05A - One sample)
a. Inspection Scope The inspectors completed one annual fire drill observation inspection sample. The
inspectors observed a fire brigade drill on September 17, 2008, in the Unit 1 turbine
building. The inspectors observed brigade performance during the drill to evaluate
donning and use of protective equipment and self-contained breathing apparatus, fire
brigade leader command and control, fire brigade response time, communications, and
the use of pre-fire plans. The inspectors attended the post-drill critique and reviewed the
disposition of issues and deficiencies identified during the drill.
b. Findings No findings of significance were identified.
1R06 Flood Protection Measures (71111.06 - One sample)
a. Inspection Scope
The inspectors completed one internal flooding sample. The inspectors reviewed the
individual plant examination and
- UFS [[]]
AR for Unit 1 concerning internal flooding events and
completed walkdowns of one area in which flooding could have a significant impact on
risk. The
RB northwest corner room were reviewed. b. Findings No findings of significance were identified.
1R07 Heat Sink Performance (71111.07A - One sample)
a. Inspection Scope The inspectors reviewed maintenance records for Unit 1 102 EDG cooling water heat
exchangers 79-03 and 79-04, performed in accordance with N1-MPM-079-412, "Diesel Generator Cooling Water Heat Exchanger and Temperature Control Valve Maintenance."
The inspectors reviewed EDG performance data to verify that heat exchanger operation
was consistent with the design basis. The inspectors interviewed the system engineer to
verify overall condition of the heat exchangers. b. Findings No findings of significance were identified. 1R11 Licensed Operator Requalification Program (71111.11Q - Two samples) a. Inspection Scope
The inspectors evaluated two simulator scenarios in the licensed operator requalification
training (LORT) program. The inspectors assessed the clarity and effectiveness of
communications, the implementation of appropriate actions in response to alarms, the
performance of timely control board operation, and the oversight and direction provided by
the shift manager. During the scenario, the inspectors also compared simulator
performance with actual plant performance in the control room. The following scenarios
were observed:
- On August 26, 2008, the inspectors observed Unit
- 1 LO [[]]
RT to assess operator and instructor performance during a scenario involving a main generator hydrogen seal oil pump failure, a grid transient that resulted in a loss of offsite 115 kV power with failure
of the 103 EDG to start, a loss of coolant accident, and failure of the reactor vessel
fuel zone water level indicator. The inspectors evaluated the performance of risk
significant operator actions including the use of special operating procedures (SOPs)
and emergency operating procedures (EOPs).
- On 5 September, 2008, the inspectors observed Unit
- 2 LO [[]]
RT to assess operator and instructor performance during a scenario involving a loss of drywell cooling, a loss of normal power to the Division 1 and 3 electrical busses, high motor temperature on one
of the operating reactor feedwater pumps that led to loss of the pump, and a loss of
coolant accident in the drywell along with failure of all reactor pressure vessel (RPV)
level indication, requiring RPV flooding. The inspectors evaluated the performance of
risk significant operator actions including the use of
EOPs.
b. Findings No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12Q - Three samples)
a. Inspection Scope The inspectors reviewed performance-based problems and the performance and condition
history of selected systems to assess the effectiveness of the maintenance program. The
inspectors reviewed the systems to ensure that the station's review focused on proper
maintenance rule scoping in accordance with 10 CFR Part 50.65, characterization of
reliability issues, tracking system and component unavailability, and 10 CFR Part 50.65
(a)(1) and (a)(2) classification. In addition, the inspectors reviewed the site's ability to
identify and address common cause failures and to trend key parameters. The following
four maintenance rule inspection samples were reviewed:
- Unit 1 125 volt
UPS) equipment issues; * Unit 2 control building heating, ventilation, and air conditioning (HVAC) system based on equipment problems that developed following implementation of a modification; and * Unit 2 reactor recirculation system based on recirculation pump seal leakage issues. b. Findings No findings of significance were identified. 1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - Six samples)
a. Inspection Scope The inspectors evaluated the effectiveness of the maintenance risk assessments required
by 10 CFR Part 50.65 (a)(4). The inspectors reviewed equipment logs, work schedules,
and performed plant tours to verify that actual plant configuration matched the assessed
configuration. Additionally, the inspectors verified that risk management actions for both
planned and emergent work were consistent with those described in station procedures.
The inspectors reviewed risk assessments for the activities listed below. Unit 1
10 * Week of July 14, 2008, that included a rebuild of 112 core spray topping pump, 13 turbine building closed loop cooling system heat exchanger cleaning, and emergent
maintenance to troubleshoot a trip of the 13 instrument air (IA) compressor, combined
within a scheduled maintenance period. * Week of July 21, 2008, that included 112 containment spray raw water system maintenance and quarterly surveillance,
UPS 162B that resulted in a half scram signal, and loss of flow monitoring capability for the electromatic relief valves and safety
valves due to a failed power supply. * Week of August 18, 2008, that included maintenance on the
RRP, and emergent maintenance to
replace the
- 103 EDG raw water pump due to low discharge pressure. Unit 2 * Week of July 14, 2008, that included Division 1
EDG monthly surveillance, residual heat removal (RHR) 'A' quarterly surveillance, replacement of unannealed red brass
piping in the IA system, and emergent maintenance to troubleshoot a level control
problem with the 2B low pressure FWH, and troubleshooting activities associated with
a radioactive waste sump pump that resulted in multiple plant equipment issues and
required a power reduction to 50 percent. * Week of July 21, 2008, that included
EDG for a two year surveillance, and
emergent maintenance to troubleshoot Division
- FWH , and a leak from the low pressure core spray pressure maintenance (keepfill) pump mechanical seal water supply. * Week of August 4, 2008, that included inspection of the 'B'
IA compressor, weld repair of the 'C' IA receiver, a three day maintenance
period on the
RCIC quarterly surveillance.
b. Findings
Introduction. An
NCV of 10 CFR 50.65(a)(4) was identified for inaccurate risk assessments completed for August 5 and 6, 2008. Specifically, the
unavailable reactor core isolation cooling (RCIC) system was not properly incorporated
into the risk assessment. Description. During the week of August 4, 2008, the
- RC [[]]
IC system was made inoperable and unavailable on several occasions for planned maintenance activities. When the
inspectors reviewed
would be inoperable and unavailable and that the value for daily CDF risk was indicated to
be "Low." The inspectors questioned this, based on previous experience when
- RC [[]]
- RC [[]]
IC was
inoperable and unavailable. Prior to this determination,
- RC [[]]
IC had been inoperable and
unavailable on two occasions during the week, with a total unavailability time of
approximately 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> (hrs). The cause of the incorrect risk assessment was determined to be that a typographical
error had been made on June 30, 2008, while entering a change to the risk monitor
computer software. This resulted in an error in the coding used to map
- RC [[]]
unavailability to risk importance in the Unit 2 PRA model, incorrectly giving it a zero risk
importance. As corrective actions, the modeling of
- RCIC was corrected and a verification of all mapping codes used in the risk monitor was performed. This issue was entered into the corrective action program (
CAP) as CR 2008-6363. The performance deficiency associated with this event was that inaccurate information
was entered in the risk monitor software resulting in an inadequate risk assessment being
used while the
- RC [[]]
IC system was inoperable and unavailable during the August 4, 2008
work week. Analysis. The finding was greater than minor because it was similar to
RCIC system maintenance was
inadequate (i.e., it underestimated the risk because of personnel error) because relevant
information provided to the risk assessment tool was inaccurate. As a result, the overall
elevated plant risk, when correctly assessed, put the plant into a higher licensee-
established risk category. Per IMC 0609, Attachment 4, Phase 1, "Initial Screening and
Characterization of Findings," the finding was evaluated in accordance with IMC 0609,
Appendix KProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix K" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., "Maintenance Risk Assessment and Risk Management Significance
Determination Process." The baseline (zero-maintenance) core damage frequency was
1.35E-5/year (yr) and the actual core damage frequency (with
- RC [[]]
IC unavailable) was
5.10E-5/yr. Therefore, the actual incremental core damage frequency was (5.10 - 1.35)E-
5/yr = 3.75E-5/yr, and the actual incremental core damage probability (ICDPactual) was (3.75E-5/yr x 30 hrs) / 8760 hrs/yr = 1.28E-7. Although a risk assessment had been
performed, the value was essentially the zero-maintenance core damage frequency; that
is, it was evaluated the same as if a risk assessment had not been performed. Therefore,
the incremental core damage probability deficit (ICDPD) was equal to
ICDPD was less than 1E-6, the finding was determined to be of very low safety
significance (Green). The finding had a cross-cutting aspect in the area of human performance because
- NMP [[]]
NS did not appropriately plan work activities by incorporating valid risk insights (H.3.a
per
CFR 50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear power plants," subsection (a)(4) states, in part, "Before performing
maintenance activities . . . the licensee shall assess and manage the increase in risk that
may result from the proposed maintenance activities. The scope of the
assessment may be limited to structures, systems, and components that a risk-informed evaluation process has shown to be significant to public health and safety." The
- NMP [[]]
- 2 RC [[]]
IC system as a high safety significant
system. Contrary to the above, on August 8, 2008, it was identified that
- NMP [[]]
NS had not correctly
assessed the risk associated with maintenance activities on August 5 and August 6 that
had made the Unit
CDF risk
had been determined to be "Low" when the actual value was "Medium." Because this
violation is of very low safety significance and was entered into the
CR 2008-
6363, this violation is being treated as an
- RC [[]]
IC Unavailability) 1R15 Operability Evaluations (71111.15 - Seven samples) a. Inspection Scope The inspectors evaluated the acceptability of operability evaluations, the use and control
of compensatory measures, and compliance with technical specifications (TSs.) The
evaluations were reviewed using criteria specified in NRC Regulatory Issue Summary
2005-20, "Revision to Guidance Formerly Contained in NRC Generic Letter 91-18,
'Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution
of Degraded and Nonconforming Conditions and on Operability'," and Inspection Manual
Part 9900, "Operability Determinations and Functionality Assessments for Resolution of
Degraded or Nonconforming Conditions Adverse to Quality or Safety." The inspectors'
review included verification that the operability determinations were made as specified by
Procedure
OP-1.01-1002, "Conduct of Operability Determinations / Functionality
Assessments." The technical adequacy of the determinations was reviewed and compared to the
UFSAR, and associated design basis documents (DBDs). The following evaluations were reviewed:
- CR 2008-5852 concerning the operability of the Unit 1 drywell equipment drain tank input to the drywell leak detection system, in light of anomalous tank level and leak rate indications; *
- 2 EDG in the emergency mode with a failed overspeed butterfly valve limit switch that had caused the
- CR 2008-5885 concerning the effect of increased Unit 2 suppression pool leakage on emergency core cooling system pump operability; and *
CR 2008-6647 concerning low peak firing pressure on one cylinder for the Unit 2 Division 3 EDG.
b. Findings
13
No findings of significance were identified. 1R18 Plant Modifications (71111.18 - Four samples)
a. Inspection Scope The inspectors reviewed a Unit 2 temporary modification to raise the 'D' service water
pump outboard bearing temperature setpoint from 130 degrees Fahrenheit (F) to 150 F.
The setpoint was raised to allow for new packing run-in on the pump. The inspectors
reviewed the 10 CFR Part 50.59 screening against the system design bases
documentation to verify that the modification did not affect system operability. The
inspectors reviewed the vendor manual to verify that increased temperature would not
affect the pump's reliability.
The inspectors reviewed a Unit 2 temporary modification that installed temporary power to
the B-phase main transformer cooling pumps and fans from the installed spare 'D' main
transformer. The inspectors reviewed the at-risk activity work package, interviewed the system engineer, and reviewed the 10 CFR Part 50.59 screening against the system design bases documentation to verify that the modification did not affect system
operability. The inspectors also reviewed the WO that installed and removed the
temporary power and walked down the equipment after work completion to verify that the
equipment had been returned to its original configuration.
b. Findings
No findings of significance were identified.
.2 Permanent Modifications
a. Inspection Scope The inspectors reviewed Unit 2 design change package (DCP) N2-99-032, "Gaseous
Effluent Monitoring System Replacement." The purpose of this modification was to replace an aging system for which system reliability had been degrading. The inspectors
assessed the adequacy of the modification package and procedural changes, verified that
applicable design and licensing basis requirements were met, and verified that design
margins were not degraded by the modification.
The inspectors reviewed Unit
CRD)
Timing Recorders at NMP1." The purpose of this modification was to improve the process
by which data is acquired and analyzed for all control rod movement. The inspectors
assessed the adequacy of the modification package and 10 CFR Part 50.59 screening, verified that applicable design and licensing basis requirements were met, and verified that design margins were not degraded by the modification. The inspectors interviewed
engineers involved with the project, walked down the system, and reviewed the post-
14maintenance test (PMT) results to verify proper installation and the test acceptance criteria
had been met. The inspectors also reviewed the affected procedures and drawings to
verify that affected documents were being updated.
b. Findings
No findings of significance were identified. 1R19 Post Maintenance Testing (71111.19 - Seven samples)
a. Inspection Scope The inspectors reviewed the PMTs listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed the test
procedure to verify that the procedure adequately tested the safety functions that may
have been affected by the maintenance activity, that the acceptance criteria in the
procedure were consistent with information in the applicable licensing basis and/or DBDs,
and that the procedure had been properly reviewed and approved. The inspectors also
witnessed the test or reviewed test data, to verify that the test results adequately
demonstrated restoration of the affected safety functions. . * Unit 1,
EPM-UPS-003, "UPS 10
Year Maintenance," and a 24-hour confidence run. * Unit 1,
PMT was performed in accordance with N1-ST-Q1C, "Core Spray 112 Pump and Valve
Operability Test," and N1-PM-V2, "Pump Curve Validation Test." * Unit 1,
PMT was performed in accordance with N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability
Test - Division I and II."
- Unit 2,
SWP*P1D. The PMT was
15performed in accordance with N2-OSP-SWP-@001, "Service Water Pump Curve
Validation Test."
b. Findings No findings of significance were identified. 1R22 Surveillance Testing (71111.22 - Eight samples)
a. Inspection Scope The inspectors witnessed performance of and/or reviewed test data for risk-significant
surveillance tests to assess whether the components and systems tested satisfied design and licensing basis requirements. The inspectors verified that test acceptance criteria
were clear, demonstrated operational readiness and were consistent with the DBDs; that
test instrumentation had current calibrations and the range and accuracy for the
application; and that tests were performed, as written, with applicable prerequisites
satisfied. Upon test completion, the inspectors verified that equipment was returned to the
status specified to perform its safety function.
The following surveillance tests were reviewed: * N1-ST-Q2, "Control Rod Drive Pumps Flow Rate Test;" * N1-ST-Q13, "Emergency Service Water Pump Operability Test;" * N1-ST-M4A, "EDG 102 and
- ST -Q6A, "Containment Spray System Loop 111 Quarterly Operability Test;" * N2-PM-A006, "B.5.b Pump Annual Flow Rate Test;" * N2-OSP-ICS-Q@002, "RCIC Pump and Valve Operability Test and System Integrity Test and
- ASME [[]]
TSP-HVC-R@001, "Testing and Analysis of Unit 2 Control Room Outdoor Air Special Filter Train System." b. Findings No findings of significance were identified.
16 Cornerstone: Emergency Preparedness
- 1EP 2 Alert and Notification System Evaluation (71114.02 - One sample) a. Inspection Scope An onsite review was conducted to assess the maintenance and testing of the
alert and notification system (ANS), including both the system sirens and tone alert radios.
During this inspection, the inspectors interviewed emergency preparedness (EP) staff
responsible for implementation of the ANS testing and maintenance. The inspectors
reviewed
- NMP [[]]
NS's corrective actions.
The inspectors further discussed the ANS with the assigned technical specialist, reviewing
system performance from June 2006 through June 2008. The inspectors reviewed the
- NMP [[]]
NS's compliance with those
commitments for system maintenance and testing. Additionally, the inspectors reviewed
changes to the design report and how these changes were captured. The Planning
Standard,
CFR Part 50, Appendix E, were used as reference criteria. b. Findings No findings of significance were identified.
1EP3 Emergency Response Organization Staffing and Augmentation System (71114.03 - One sample)
a. Inspection Scope The inspectors conducted a review of the
- NMP [[]]
NS emergency response organization
(ERO) augmentation staffing requirements and the process for notifying and augmenting
the ERO. This was performed to ensure the readiness of key staff for responding to an
event and to ensure timely facility activation. The inspectors reviewed procedures and
ERO notification system and drills, and reviewed records from
call-in drills. The inspectors interviewed personnel responsible for testing the ERO
augmentation process, and reviewed the training records for a sampling of ERO to ensure
training and qualifications were up to date. The inspectors reviewed procedures for ERO
administration and training, and verified a sampling of ERO participation in exercises and
drills in 2007 and 2008. The Planning Standard,
CFR Part 50, Appendix E, were used as reference criteria. b. Findings No findings of significance were identified.
17
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - One sample)
a. Inspection Scope Prior to this inspection, the
NMPNS developed these changes in accordance with 10 CFR Part 50.54(q), and determined that the changes did
not result in a decrease in effectiveness of the
- NMP [[]]
CFR Part
50.47(b) and Appendix E to 10 CFR Part 50. During this inspection, the inspectors
conducted a review of
CFR Part 50.54(q) screenings for all the changes made to the emergency action levels (EALs) and all of the changes made to the Plan from
August 2007 through June 2008 that could have potentially resulted in a decrease in effectiveness of the Plan. This review of the
NRC approval of the changes and, as such, the changes remain subject to future NRC
inspection. The requirements in 10 CFR Part 50.54(q) were used as reference criteria.
b. Findings No findings of significance were identified.
1EP5 Correction of Emergency Preparedness Weaknesses (71114.05 - One sample)
a. Inspection Scope The inspectors reviewed a sampling of self-assessment procedures and reports to assess
concerning drills, self-assessments, and audits. Additionally, the inspectors reviewed:
- EP Oversight Board meeting minutes; Quality and Performance Assurance reports; event reports for the September 2007 Alert and the May 2008 Unusual Event declarations at
CFR Part
50.47(b)(14), and the related requirements of 10 CFR Part 50, Appendix E, were used as
reference criteria.
b. Findings No findings of significance were identified.
1EP6 Drill Evaluation (71114.06 - One sample)
a. Inspection Scope The inspectors observed control room operator emergency plan response actions during
the Unit 2 evaluated
- LO [[]]
RT scenario on September 5, 2008. The inspectors verified that
emergency classification declarations and notifications were completed in accordance with
CFR Part 50 Appendix E, and the emergency implementing
procedures.
b. Findings
No findings of significance were identified. 2.
- RADIAT [[]]
- ION [[]]
OS1 Access Control to Radiologically Significant Areas (71121.01 - Six samples)
a. Inspection Scope The inspectors reviewed radiation work permits for airborne radioactivity areas with the potential for individual worker internal exposures of greater than 50 millirem (mrem)
committed effective dose equivalent (20 derived air concentration (DAC)-hours). For
these selected airborne radioactive material areas, the inspectors verified barrier integrity
and engineering controls performance (e.g., high efficiency particulate air ventilation
system operation). The inspectors reviewed and assessed the adequacy of
- NMP [[]]
NS's internal dose
assessment for any actual internal exposure greater than 50 mrem committed effective dose equivalent. The inspectors examined
- NMP [[]]
NS's physical and programmatic controls for highly
activated or contaminated materials (non-fuel) stored within the spent fuel pools.
The inspectors discussed with the acting radiation protection manager high dose rate-high
radiation area, and very high radiation area controls and procedures. The inspectors
focused on any procedural changes since the last inspection. The inspectors verified that
any changes to
- NMP [[]]
NS's procedures did not substantially reduce the effectiveness and level of worker protection. The inspectors discussed with health physics supervisors the controls in place for special
areas that have the potential to become very high radiation areas during certain plant
operations. The inspectors determined if these plant operations required communication
beforehand with the health physics group, so as to allow corresponding timely actions to
properly post and control the radiation hazards. The inspectors verified adequate posting and locking of all entrances to high dose rate-
high radiation areas, and very high radiation areas.
The inspectors evaluated
19 b. Findings
No findings of significance were identified.
ALARA Planning and Controls (71121.02 - Four samples)
a. Inspection Scope The inspectors reviewed the results of the Spring 2008 Unit 2 refueling outage (2RFO11),
including the causes of any radiologically significant work (greater than five person-rem
collective exposure) which exceeded its dose estimate.
The inspectors obtained from
- NMP [[]]
NS a list of work activities ranked by actual/estimated exposure that are in progress or that have been completed during the last outage and
selected the two work activities of highest exposure significance.
The inspectors reviewed the as low as reasonably achievable (ALARA) work activity evaluations, exposure estimates, and exposure mitigation requirements. The inspectors
determined if
- NMPNS had established procedures, engineering and work controls, based on sound radiation protection principles to achieve occupational exposures that were
- NMP [[]]
NS had reasonably grouped the radiological
work into work activities, based on historical precedence, industry norms, and/or special circumstances. The inspectors compared the results achieved (dose rate reductions, person-rem used)
with the intended dose established in
ALARA planning for these work activities.
The inspectors reviewed the assumptions and basis for the current annual collective
exposure estimate. The inspectors reviewed applicable procedures to determine the
methodology for estimating work activity-specific exposures and the intended dose outcome. The inspectors evaluated both dose rate and man-hour estimates for
reasonable accuracy. The inspectors reviewed
- NMP [[]]
NS's method for adjusting exposure estimates, or re-
planning work, when unexpected changes in scope or emergent work are encountered.
The inspectors determined if adjustments to estimated exposure (intended dose) were
based on sound radiation protection and
- ALA [[]]
RA principles or just adjusted to account for
failures to control the work.
The inspectors evaluated
CFR Part 20.1101.
b. Findings
No findings of significance were identified.
20
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - One sample)
a. Inspection Scope The inspectors reviewed the plant
- UFS [[]]
AR to identify applicable radiation monitors
associated with transient high and very high radiation areas including those used in
remote emergency assessment.
The inspectors evaluated
- NMP [[]]
CFR Part 20.1703 and 10 CFR Part 20.1704.
b. Findings
No findings of significance were identified. 4.
- OTHER [[]]
- 4OA 1 Performance Indicator Verification (71151 - Seven samples) a. Inspection Scope The inspectors sampled
PI definition
guidance contained in Nuclear Energy Institute (NEI) 99-02, "Regulatory Assessment
Performance Indicator Guideline," Revision 5, was used to verify the basis in reporting for
each data element.
Cornerstone: Initiating Events
The inspectors reviewed licensee event reports (LERs) and operator logs to determine
whether
- NMP [[]]
NS accurately reported the number of unplanned power changes greater
than 20 percent at Unit 1 and Unit 2 from October 2007 to June 2008.
- Unit 1 unplanned power changes per 7000 critical hours * Unit 2 unplanned power changes per 7000 critical hours Cornerstone: Mitigating Systems
Unit 1 and Unit 2 LERs issued between the end of the third quarter 2007 and the end of
the second quarter 2008 were reviewed for safety system functional failures.
- Unit 1 safety system functional failures * Unit 2 safety system functional failures
21 Cornerstone: Emergency Preparedness The inspectors reviewed data for the
- EP [[]]
ANS Reliability. The inspectors reviewed the PI data, its
supporting documentation, and the information
- NMP [[]]
NS reported for the third and fourth
quarters of 2007, and the first and second quarters of 2008, to verify the accuracy of the
reported data. The acceptance criteria used for the review were 10 CFR Part 50.9 and
Additionally, the inspectors performed
TI, and forwarded that
data to
OA2 Identification and Resolution of Problems (71152 - Two samples) .1 Review of Items Entered into the CAP
a. Inspection Scope As specified by Inspection Procedure 71152, "Identification and Resolution of Problems,"
and in order to help identify repetitive equipment failures or specific human performance
issues for follow-up, the inspectors performed a daily screening of items entered into
CAP. In accordance with the baseline inspection procedures, the inspectors
also identified selected CAP items across the initiating events, mitigating systems, and barrier integrity cornerstones for additional follow-up and review. The inspectors assessed
the threshold for problem identification, the adequacy of the cause analyses, extent of
condition review, operability determinations, and the timeliness of the specified corrective
actions.
b. Findings No findings of significance were identified.
.2 Annual Sample - Review of Corrective Actions for Unit 1 Feedwater Heater Issues
a. Inspection Scope This inspection focused on
- NMP [[]]
NS's problem identification, evaluation, and resolution of
a Unit 1 level control valve (LCV)-26-09 actuator o-ring issue associated with the 122
FWH tripped on high-high level when LCV-26-09
failed in the closed position and caused a cascading affect that backed up the water flow
to the other
FWHs tripped due to high-
high level within 30 minutes, and the last FWH in the heater string (125) tripped several
2hours later. This caused operators to reduce reactor power to less than 80 percent and
produced significant water-hammer in the FWH system piping. Following this event,
operators initiated a condition report (CR 2007-5475) to resolve the issue.
- NMP [[]]
NS
performed corrective maintenance on the valve actuator o-ring and repaired damaged
piping and supports on the 12 heater string prior to returning the system to service.
The inspectors selected the FWH issue for review because it resulted in an unplanned
reactivity change and power reduction, caused significant water-hammer in the system,
and challenged plant operators. The inspectors reviewed
- NMP [[]]
NS's associated
troubleshooting results, root cause evaluation, extent of condition review, and short-term and long-term corrective actions. The inspectors conducted a walkdown of accessible portions of the system, and reviewed the material condition of the LCVs, design control
measures, and configuration control. The inspectors also interviewed plant personnel and
reviewed procedures, related industry operating experience (OE), and the vendor manual
for the
- FWH [[]]
- NMPNS [[]]
NMPNS operated and maintained the FWH system as required.
b. Assessment and Observations
No findings of significance were identified.
- NMP [[]]
NS used a failure modes and effects
analysis in the root cause evaluation to determine the nature of the LCV malfunction. The
root cause evaluation determined that the lubricant used in the actuator degraded to the
point where it caused the actuator o-rings to harden, thereby allowing air to leak past the
actuating piston. This caused insufficient air pressure to the valve actuator such that it
would not open the
performed a thorough review of the issue and implemented appropriate corrective actions.
The corrective actions were aligned with the root cause analysis and included procedure
and preventive maintenance revisions, implementing the use of a new lubricant, improved training to operators and engineering personnel on water-hammer mechanisms, and
operating experience program improvements. The inspectors concluded that
CAP. The
inspectors also determined that the root cause evaluation and subsequent follow-up
corrective maintenance were generally sufficient and based on the best available
information, troubleshooting, and relevant industry
NMPNS's assigned
corrective actions were adequately tracked, appropriately documented, and completed as
scheduled.
.3 Annual Sample - Review of Corrective Actions for Inadvertent Carbon Dioxide (CO2) Discharge
a. Inspection Scope The inspectors reviewed
- NMP [[]]
NS's evaluation and corrective actions associated with the
September 19, 2007 inadvertent discharge of
CR 2007-5538). The event occurred during
an installation of wiring in a local fire panel as part of a design change, and resulted in
NMPNS's root cause
analysis and corrective actions to ensure that appropriate evaluations were performed and
23corrective actions were specified and prioritized. The inspectors also reviewed the follow-
up actions to verify that the root cause and corrective actions identified were addressed.
b. Findings & Observations No findings of significance were identified. The inspectors determined that, in general, the
corrective actions taken associated with the inadvertent CO2 discharge were reasonable
and adequate. 4OA3 Followup of Events and Notices of Enforcement Discretion (71153 - Three samples)
.1 (Closed) LER 05000220/2008-001-00, Loss of Offsite Power due to an Equipment Malfunction On May 13, 2008, a loss of Unit 1 offsite power occurred due to an offsite equipment
failure which caused a loss of 115 kV offsite power line 4 while the remaining 115 kV
offsite power line (line 1) was removed from service for planned maintenance. The event
detailed in this
OA3 of Inspection Report
05000220/2008003. The inspectors reviewed this LER and no findings of significance
were identified. This LER is closed.
.2 (Closed)
- LER 05000410/2008-001-00, Unqualified Relays Installed Since Original Construction Result in an Unanalyzed Condition On April 10, 2008,
NMPNS discovered that the J10 alarm relays in RB ventilation system
unit cooler motor starter circuits did not satisfy the environmental qualification
requirements of 10 CFR 50.49. This discovery came as a result of investigation of the
cause of J10 relay failures during loss of offsite power testing that was performed during
the 2008 refueling outage. J10 relay failures resulted in an NCV as documented in
Section 1R22 of Inspection Report 05000410/2008003. The inspectors reviewed this LER
and no additional findings of significance were identified. The failure of the J10 relays to
meet the environmental qualification requirements of 10 CFR 50.49 constitutes a violation
of minor significance that is not subject to enforcement action in accordance with Section
LER is closed. .3 Power Reduction due to a Maintenance-Related Electrical Transient
a. Inspection Scope On July 14 at 1:12 p.m., Unit 2 experienced a partial loss of feedwater heating due to loss
of extraction steam to the 6B (high pressure) and 5C (low pressure) FWHs. The cause of
the event was an unrelated maintenance activity that unexpectedly produced an electrical
transient which affected a number of plant systems. Other consequences of the transient
were loss of the 'A' and 'C' heater drain pumps, loss of the 'B' offgas train, loss of normal
RB and start of the standby gas
treatment system, and isolation of the hydrogen water chemistry system.
24Operators responded in accordance with N2-SOP-08, "Unplanned Power Changes," and
N2-SOP-101D, "Rapid Power Reduction," to lower reactor power to 73 percent. After the
cause of the transient was identified, operators commenced recovery of the FWHs. While
attempting to restore the 5C FWH to service, resultant system perturbations caused an
isolation of the 6C
FWHs (6B and 6C) out of service, N2-
SOP-08 directed that an orderly plant shutdown be commenced. Operators resumed
power reduction until, at 50 percent power, the 6B FWH was successfully returned to
service. The plant shutdown was terminated and power ascension commenced in
coordination with restoration of the remaining affected systems. Power was restored to
full RTP on July 15. The inspectors responded to the control room and observed operators' responses to the
event, and reviewed the circumstances surrounding the event.
b. Findings Introduction. A self-revealing Green finding was identified on July 14, 2008, when inadequate maintenance practices, during replacement and troubleshooting of a Unit 2
radioactive waste sump pump, caused an electrical transient that resulted in the loss of
numerous plant components and required a power reduction. Description. In May of 2008, radioactive waste sump pump
WO required that a rotation check be performed after the
electrical terminations had been completed. This, however, was not done because the
need for it was not recognized until after the pump had been installed in the sump.
Although work was stopped to determine a course of action, the pump remained available
for automatic operation as the backup sump pump. On July 8, 2008, it was recognized
that the pump had run several times since the work had been stopped, as indicated by the
pump run chart. This was incorrectly used to verify proper pump operation, and the
rotation check and
WO were signed off as complete. On July 9, 2DFW-P1A was discovered to be running with no discharge pressure. In
developing a troubleshooting plan,
- NMP [[]]
NS initial actions were to reverse power leads to
the pump. During testing the pump had no discharge pressure and, after two minutes, tripped on thermal overload. The leads were returned to the original configuration, and the pump was again energized by closing its circuit breaker on motor control center (MCC)
MCC016. Shortly after the breaker was shut, noise was heard and flame was
observed coming from the breaker cubicle. The feeder breaker from power board
US9,
caused by this failure (a short), resulted in the equipment losses discussed above. In response to this event, the fire brigade responded to a fire alarm in the vicinity of
DFW-P1A. Operators responded to the partial loss of feedwater heating by reducing power to 73
percent. This issue was entered into the
CR 2008-5745. The cause of the event was that the pump suction and discharge were plugged with debris
from the sump, which resulted in high motor current due to the pump being in a bound
25rotor condition. This, combined with a manufacturing defect associated with wiring
insulation in the breaker, resulted in a phase-to-ground short between the breaker and the
motor control center. The performance deficiency associated with this event was inadequate maintenance
practices. Specifically: Following replacement in May, the pump was left in a condition
such that it would operate automatically prior to the performance of
GAP-SAT-02, "Pre/Post-Maintenance Test Requirements," Revision
27, states that the
- PMT shall check components that were affected by the maintenance, verify that maintenance was properly performed, and verify that a new deficiency was not created. Had
PMT been performed at the time of installation, low flow would likely have
shown that the pump discharge piping was already plugged with sump debris. This would
have prevented continued use of the pump and prevented subsequent troubleshooting
from focusing on the direction of motor rotation. Additionally: The troubleshooting plan
was inadequate in that, even if the pump had been rotating backwards, it would have
developed some discharge pressure; and, after the phase reversal had produced no
change in pump performance, the motor was restored to its original configuration and
tested, rather than to have reevaluated the troubleshooting plan. Constellation procedure
MN-1.01-1002, "Troubleshooting," Revision 0001, requires that troubleshooting shall
be stopped in the event of an unexpected equipment response, and that the
troubleshooting plan shall be reevaluated accordingly. Analysis. The finding was greater than minor because it was similar to IMC 0612, Appendix E, example 4.b, in that the inadequate maintenance resulted in a plant transient
that affected multiple systems and components. The finding affected the human
performance attribute of the Initiating Events cornerstone objective to limit the likelihood of
those events that upset plant stability and challenge critical safety functions during
shutdown as well as power operations. The finding was evaluated in accordance with IMC
0609, Attachment 4, and determined to be of very low safety significance (Green) per the
SDP Phase one determination because the finding did not contribute to both the likelihood
of a rector trip and the likelihood that mitigation equipment or functions would not be
available, and did not screen as potentially risk significant due to external events. The finding had a cross-cutting aspect in the area of human performance because
- NMPNS did not appropriately plan the pump troubleshooting activity by incorporating abort criteria (H.3.a per
IMC 0305). Enforcement. No violation of regulatory requirements occurred. The inspectors determined that the finding did not represent a noncompliance issue because it occurred on non safety-class balance of plant equipment. (FIN 05000410/2008004-02, Inadequate Maintenance Practices Result in a Plant Transient)
26 4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
a. Inspection Scope During the inspection period, the inspectors conducted observations of security force
personnel and activities to ensure that the activities were consistent with
- NMP [[]]
NS's security procedures and regulatory requirements relating to nuclear plant security. These
observations took place during both normal and off-normal plant working hours.
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an
integral part of the inspectors' normal plant status review and inspection activities.
b. Findings
No findings of significance were identified.
- 4OA 6 Meetings, including Exit Exit Meeting Summary The inspectors presented the inspection results to Mr. Keith Polson and other members of
- ATTACH [[]]
- MENT [[:]]
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- ATION [[]]
- KEY [[]]
- POINTS [[]]
- OF [[]]
CONTACT Licensee Personnel
S. Belcher, Plant Manager
W. Byrne, Manager, Nuclear Security
R. Dean, Director, Quality and Performance Assessment
T. Inc, I&C Technician
J. Kaminski, Manager, Emergency Preparedness
J. Krakuszeski, Manager, Operations
J. Laughlin, Manager, Engineering Services
K. Polson, Vice President
J. Schultz, Chemistry Supervisor, J.A. FitzPatrick Nuclear Power Plant
T. Shortell, Manager, Training
S. Sova, Manager, Radiation Protection K. Stoffle, Environmental Support Supervisor J. Stone, Chemistry Technician
- LIST [[]]
- OF [[]]
- ITEMS [[]]
- AND [[]]
- DISCUS [[]]
RCIC Unavailability (Section 1R13)05000410/2008004-02
OA3)
Closed
05000220/2008-001-00
OA3)
05000410/2008-001-00 LER Unqualified Relays Installed Since Original Construction Result in an Unanalyzed
Condition (Section 4OA3)
Discussed
None.
A-2Attachment
- LIST [[]]
- OF [[]]
- DOCUME [[]]
- NTS [[]]
- REVIEW [[]]
ED Section 1R01: Adverse Weather Protection S-ODP-OPS-0112, "Offsite Power Operations and Interface," Revision 12
N1-SOP-33A.3, "Major 115 KV Grid Disturbances," Revision 01
N2-SOP-70, "Major Grid Disturbances," Revision 01
EPP-26, "Natural Hazard Preparation and Recovery," Revision 01
N1-OP-64, "Meteorological Monitoring," Revision 01
N2-OP-102, "Meteorological Monitoring," Revision 04
Section 1R04: Equipment Alignment N2-ELU-01, "Walkdown Order Electrical Lineup and Breaker Operations," Revision 00
N1-OP-18, "Service Water System," Revision 02
- SD [[]]
BD-502, "Service Water System Design Basis Document," Revision 07
N1-ST-Q13, "Emergency Service Water Pump Operability Test," Revision 11
N1-ST-V14, Service Water Check Valve And Emergency Service Water Pump and Check
Valve Test," Revision 03
N2-OP-33, "High Pressure Core Spray System," Revision 07
N2-VLU-01, "Walkdown Order Valve Lineup and Valve Operations," Attachment 33, "N2-OP-33 Walkdown Valve Lineup," Revision 00
Piping and Instrumentation Diagram (P&ID)-33, "High Pressure Core Spray System" Section 1R05: Fire Protection
- CM [[]]
UFSAR, Appendix 9B, "Safe Shutdown Evaluation"
N2-FPI-PFP-0201, "Unit 2 Pre-Fire Plans," Revision 0
Section 1R06: Flood Protection Measures Internal Flooding Analysis Notebook, Nine Mile Point Unit 1, Revision 00
Nine Mile Point Nuclear Station - Unit 1 Individual Plant Examination, July 1993
N1-PM-V-29, "Reactor Building Sump Pump System Operability Test," Revision 00
CR 2006-5956
ACR 06-06589
Section 1R07: Heat Sink Performance S15-79-HTX03, "Replacement Emergency Diesel Generator Raw Water Heat Exchanger
Design," Revision 00
S15-79-HTX-01, "Emergency Diesel Generator Cooling Water (EDGCW) Heat Exchanger
Thermal Performance Evaluation," Revision 00, Disposition 00A
A-3Attachment Section 1R11: Licensed Operator Requalification Program N1-SOP-32, "Generator Auxiliaries Failures," Revision 02
N1-SOP-33A.1, "Loss of 115 KV," Revision 01
N1-SOP-33A.3, "Major 115 KV Grid Disturbances," Revision 01
N1-EOP-2, "RPV Control," Revision 01400
N1-EOP-4, "Primary Containment Control," Revision 01400
N2-SOP-60, "Loss of Drywell Cooling," Revision 04
N2-SOP-03, "Loss of
SOP-06, "Feed Water Failures," Revision 04 N2-SOP-101D, "Rapid Power Reduction," Revision 05
N2-SOP-29, "Sudden Reduction in Core Flow," Revision 07
N2-SOP-101C, "Reactor Scram," Revision 03
N2-EOP-RPV, "RPV Control," Revision 11
N2-EOP-PC, "Primary Containment Control," Revision 12
N2-EOP-C4, "RPV Flooding," Revision 12
Section 1R12: Maintenance Effectiveness S-MRM-REL-0101, "Maintenance Rule," Revision 18
S-MRM-REL-0104, "Maintenance Rule Scope," Revision 01
S-MRM-REL-0105, "Maintenance Rule Performance Criteria," Revision 01
Control Room
- HV [[]]
AC System Health Reports, Q3-2006 through Q2-2008
N2-TSP-HVC-R@001, "Testing and Analysis of Unit 2 Control Room Outdoor Air Special Filter Train System," Revision 01 Reactor Recirculation System Health Reports, Q4-2007 through Q3-2008 T-1792, "In-Place Testing of Nuclear Air Cleaning Systems for Nine Mile Point 2" Unit 2 Maintenance Rule Scoping Document
- AS [[]]
CR 08-04282
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
PSH-03, "On-line Work Management Process," Revision 11
Section 1R15: Operability Evaluations
OP-1.01-1002, "Conduct of Operability Determinations / Functionality Assessments,"
Revision 00
A10.1-N-341, "Revise
IST Test Performance Flow Criteria from 9000 GPM to
10,000 GPM," Revision 00, Disposition 00H
N2-OSP-SWP-@001, "SW Pump Curve Validation Test," Revision 04
A-4Attachment Section R18: Plant Modifications N1-MFT-105, "Replace
- CRD Timing Recorders," Revision 01 C-22030-C, "Elementary Diagram Reactor Manual Control System," Sheet 1, Revision 33
MTX-XM1B
Second Stage Cooling Pump and Fans," Revision 0000
08-15377-00, "Implement Temp Mod to Provide to Cooling Bank Two from Transformer 1D"
EC20080016-000
Section 1R19: Post Maintenance Testing
SAT-02, "Pre/Post Maintenance Test Requirements," Revision 26
MDC-11, "Pump Curves and Acceptance Criteria," Revision 14
S15-72-F003, "IST Approved Pump Curves Emergency Diesel Generator Cooling Water,"
Revision 08
N1-MMP-079-119, "Diesel Generator Cooling Water Pumps Maintenance," Revision 02
S-TTP-PUMP-@001, "Generic Pump Curve Validation Procedure," Revision 00
N2-OSP-SWP-@001, "Service Water Pump Curve Validation Test," Revision 04
A10.1-N-341, "Revise
IST Test Performance Flow Criteria From 9,000 to 10,000
GPM," Revision 00, Disposition 00H
N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability Test - Division I
and
OPS-117, "Integrated Risk Management," Revision 14
Section
WR 82-26, "Qualification of the Oswego County Prompt Notification System for Nine Mile Point and James A. Fitzpatrick Nuclear Power Plants,"
August 1982 Wyle Research Report
- WR 84-22, "Evaluation of the Oswego County Prompt Notification System," June 1984 Public Notification System Service Manual, Federal Signal Corporation Engineered Systems
- NMPNS [[]]
- 08 NMPNS [[]]
- 24 NMPNS [[]]
EPMP-EPP-08, "Maintenance, Testing and Operation of the Oswego County Prompt Notification System," Revision 14 All siren and tone alert radio CRs dated between July 2006 and June 2008
A-5Attachment Section
- NMPNS [[]]
- NMPNS [[]]
- NMPNS [[]]
- 15 NMPNS [[]]
GAP-OPS-01, "Administration of Operations," Revision 49
Nine Mile Point Emergency Response Organization Duty Roster, Revision 2008-11
- NMP [[]]
NS Training Server Emergency Preparedness Job Matrices
Report, "Nine Mile Point Off-Hours Un-Announced All-Report Drill," October 12, 2007
CR 2008-5135
Section
NMPNS Site Emergency Plan, Revision 54
Licensing Document Change Request S-06-SEP-004 for Emergency Plan Revision 54
NMPNS Site Emergency Plan Revision 54
Change Packages for
EAL Revisions 16, 17, 18, and 19
Change Package for
- NMPNS [[]]
EPMP-EPP-01, "Maintenance of Emergency Preparedness," Revision 24, Attachment 3, "10CFR50.54(Q) Evaluation and Effectiveness Review" CR 2007-7349
10CFR50.54(q) screenings and reviews, dated between August 2007 and June 2008
Section
- NMP [[]]
NS Quality and Performance Assurance Assessment Reports:
07-037, "ERO Staffing"07-054, "Observation of the June 7, 2007, EP Drill"07-068, "Observation of the
EP Exercise and Follow-up Activities"08-005, "Use of Corrective Action Process in EP"08-006, "EAL Review"08-023, "Observation the of March 4, 2008, Drill"08-058, "Technical Support Center Focus Area Drills"08-064, "Observation of the June 26, 2008, Drill"
- NMP [[]]
- NMP [[]]
NS Report for the May 13, 2008, Unusual Event
Condition Report Summary for all
CRs dated between July 2007 and June 2008
A-6Section
- NMPNS [[]]
- EP [[]]
PI data, July 2007 - June 2008
Public Notification System
CM-1.01-1003, "Design Engineering and Configuration Control", Revision 00001
N2-ARP-1, Revision 00, Attachment 29
CON-01, "Design and Configuration Control Process," Revision 23
Safety Manual Chapter 20, Attachment 4, "Electrical Safety Checklist" WO 07-02412-18
Condition Reports 2008-5827
2008-5692
2008-5824
2008-5738
2008-6947
2008-7083
2008-7092
2008-7222
2008-7172
2008-5028
2008-6946 2008-6879 2008-6894
2008-6787
2008-6674
2008-6330
2008-4021
2008-6400
2008-6468 2008-6588
2008-6513
2008-6834
2008-7259
2004-3751
2006-1498
2006-4548
2006-4845
2006-5063
2006-5133
2006-5523
2006-5758 2007-0359 2007-0542
2007-0552
2007-1179
2007-1198
2007-5411
2007-6783 2007-7070
2008-0126
2008-0253
2008-1678
2008-1698
2008-2208
2008-3501
2008-4031
2008-4422
2008-4453
2008-5449 2008-6946 2008-7365
A-7
- LIST [[]]
- OF [[]]
- ACRONY [[]]
ALARA as low as reasonably achievable
ANS alert and notification system
CAP corrective action program
CDF core damage frequency
CFR Code of Federal Regulations
CR condition report
CRD control rod drive
DAC derived air concentration
DBD design basis document
DC direct current
DCP design change package
EAL emergency action level
EDG emergency diesel generator
ERO emergency response organization ESW emergency service water
F Fahrenheit
- HP [[]]
hr hour
- HV [[]]
AC heating, ventilation, and air conditioning
- IC [[]]
DP incremental core damage probability
IMC inspection manual chapter
kV kilovolt
LCV level control valve
- LO [[]]
RT licensed operator requalification training
MCC motor control center
mrem millirem
NCV non-cited violation
- LLC [[]]
- PA [[]]
RS Publicly Available Records
PI performance indicator
- RC [[]]
IC reactor core isolation cooling
A-8RPV reactor pressure vessel RRP reactor recirculation pump
RTP rated thermal power
SDP significance determination process
SOP special operating procedure
TI temporary instruction
- UFS [[]]
AR updated final safety analysis report
UPS uninterruptible power supply
WO work order
yr year