IR 05000263/2007004
Download: ML073040073
Text
October 30, 2007
Mr. Timothy J. O'ConnorSite Vice President Monticello Nuclear Generating Plant Nuclear Management Company, LLC 2807 West County Road 75 Monticello, MN 55362-9637
SUBJECT: MONTICELLO NUCLEAR GENERATING PLANTNRC INTEGRATED INSPECTION REPORT 05000263/2007004
Dear Mr. O'Connor:
On September 30, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed aninspection at your Monticello Nuclear Generating Plant. The enclosed integrated inspection report documents the inspection findings which were discussed on October 4, 2007, with you and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, there was one NRC-identified and two self-revealedfindings of very low safety significance, of which two involved a violation of NRC requirements.
However, because the violations were of very low safety significance and because the issues were entered into your corrective action program, the NRC is treating these findings as non-cited violations in accordance with Section VI.A.1 of the NRC's Enforcement Policy.
Additionally, two licensee-identified violations are listed in Section 4OA7 of this report.If you contest the subject or severity of a non-cited violation, you should provide a responsewithin 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -
Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of T. O'Connor-2-Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and theResident Inspector Office at the Monticello Nuclear Generating Station.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letterand its enclosure will be available electronically for public inspection in the NRC PublicDocument Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/Kenneth Riemer, ChiefBranch 2 Division of Reactor ProjectsDocket No. 50-263License No. DPR-22
Enclosure:
Inspection Report 05000263/2007004
w/Attachment:
Supplemental Informationcc w/encl:M. Sellman, President and Chief Executive OfficerD. Cooper, Senior Vice President and Chief Nuclear Officer Manager, Nuclear Safety Assessment J. Rogoff, Vice President, Counsel, and Secretary Nuclear Asset Manager, Xcel Energy, Inc.
State Liaison Officer, Minnesota Department of Health R. Nelson, President Minnesota Environmental Control Citizens Association (MECCA)
Commissioner, Minnesota Pollution Control Agency D. Gruber, Auditor/Treasurer, Wright County Government Center Commissioner, Minnesota Department of Commerce Manager - Environmental Protection Division Minnesota Attorney General's Office
SUMMARY OF FINDINGS
Inspection Report 05000263/2007004; 07/01/2007 - 09/30/2007; Monticello Nuclear GeneratingPlant. Inservice Inspection Activities, Maintenance Risk Assessments and Emergent Work
Control, Event Follow-up.This report covers a three-month period of baseline resident inspection and announcedbaseline inspections of radiation protection and inservice inspection. The inspections wereconducted by Region III reactor inspectors, a regional health physics inspector and the resident inspectors. The significance of most findings is indicated by their color (Green, White, Yellow,
Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be "Green" or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.A.NRC-Identified and Self-Revealed Findings
Cornerstone: Initiating Events
- Green.
A finding of very low safety significance was self-revealed when the 12B lowpressure feedwater heater drain valve unexpectedly closed, causing a feedwater temperature perturbation. Specifically, the drain valve closed when technicians attached calibration equipment to the instrument air supply line to the control valve, causing air pressure to decrease to the control valve actuator. The inspectors determined that the performance deficiency affected the cross-cutting area of Human Performance, having resources components, and involving aspects associated with the failure to correctly label plant components. H.2(c)]This finding was more than minor because the performance deficiency affected theprocedure quality attribute of the Initiating Events cornerstone's objective of limiting the likelihood of events that upset plant stability. The inspectors determined that the finding was of very low safety significance because it was not: (1) associated with the likelihood of initiating a loss of coolant accident; (2) did not contribute to both the likelihood of a scram and unavailability of Mitigating Systems; and (3) was not associated with a fire or flood. No violation of NRC requirements was identified. (Section 1R13)
Cornerstone: Mitigating Systems
- Green.
A finding of very low safety significance was identified by the inspectors for aviolation of 10 CFR 50, Appendix B, Criterion IX, "Control of Special Processes," associated with the licensee's failure to use a nondestructive examination (NDE)procedure qualified in accordance with Codes and Standards for detection of pitting in safety-related service water systems. Specifically, the ultrasonic (UT) examinationswere conducted by the licensee in accordance with UT Procedure PEI-02.03.12 "Ultrasonic Detection of Pitting," which was not qualified for detection of discontinuitiesin accordance with ASME Section V, "Nondestructive Examination." As a result, the licensee entered the issue into their corrective action program. The inspectors Enclosure2determined that the performance deficiency affected the cross-cutting area of HumanPerformance, having resources components and involving aspects associated with maintaining long-term plant safety by the maintenance of design margins and the minimization of long-standing equipment issues. H.2(a)]The finding was more than minor because the performance deficiency affected theprocedure quality attribute of the Mitigating Systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors applied the Inspection Manual Chapter (IMC) 0609, Appendix A, "Significance Determination of Reactor Inspection Findings for the At-Power Situations" to this finding. Under Column 2 of the Phase 1 worksheet "Mitigating Systems Cornerstone," the inspectors answered: "No" to question 1 related to design or qualification deficiencies; "No" to questions 2, 3 and 4 related to loss of train or system safety functions; and "No" to question 5 related to seismic, flooding and severe weather. Therefore, the finding was considered to be of very low safety significance. (Section 1R08)*Green. A finding of very low safety significance was self-revealed for a violation of10 CFR 50, Appendix B, Criterion V, when licensed operators failed to perform Procedure OSP-RHR-0545-02, "RHR Containment Spray/Cooling Logic Test -
Division II," in accordance with the written instructions of the procedure. Specifically, thelicensed operators landed a test jumper in the wrong electrical cabinet during the conduct of the test. Additionally, after identifying the error, the operators took actions to remove the incorrectly landed test jumper, install the test jumper at the correct location, and proceed with the test, without first notifying management. These actions were not allowed by the test procedure, nor were they in accordance with operations department standards and expectations. The inspectors determined that the performance deficiency affected the cross-cutting area of Human Performance, having decision-making components and involving aspects associated with making safety-significant or risk-significant decisions using a systematic process, especially when faced with uncertain plant conditions, to ensure safety is maintained. H.1(a)]The finding was more than minor because it affected the configuration control attributeof the Mitigating Systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined that the finding was of very low safety significance because it was not associated with a design or qualification deficiency, did not result in the loss of a train or safety system function, and was not related to a seismic, flooding, or severe weather event. (Section 4OA3.4)
B.Licensee-Identified Violations
Violations of very low safety significance, which were identified by the licensee havebeen reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.
Enclosure3
REPORT DETAILS
Summary of Plant StatusMonticello operated at full power for the entire assessment period except for brief down-powermaneuvers to accomplish rod pattern adjustments and to conduct planned surveillance testing activities.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, andEmergency Preparedness
1R01 Adverse Weather
a. Inspection Scope
The inspectors performed a detailed review of the licensee's procedures andpreparations for operating the facility during an extended period of time when ambient outside temperature was high and the ultimate heat sink (Mississippi River) wasexperiencing elevated temperatures, decreased flow rates, and below average levels.
The inspectors focused on plant specific design features and implementation of the procedures for responding to or mitigating the effects of these conditions on the operation of the facility's service water systems. Inspection activities included a review of the licensee's adverse weather procedures, daily monitoring of the off-normal environmental conditions, and that operator actions specified by plant specific procedures were appropriate to ensure operability of the facility's service water systems.The inspectors evaluated readiness for seasonal susceptibilities of the following systemsfor a total of one sample:*service water systems.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment (71111.04).1Partial Walkdown
a. Inspection Scope
The inspectors performed partial walkdowns of accessible portions of trains ofrisk-significant Mitigating Systems equipment. The inspectors reviewed equipment alignment to identify any discrepancies that could impact the function of the system and potentially increase risk. Identified equipment alignment problems were verified by the inspectors to be properly resolved. The inspectors selected redundant or backup 4systems for inspection during times when equipment was of increased importance dueto unavailability of the redundant train or other related equipment. Inspection activities included a review of the licensee's procedures, verification of equipment alignment, and an observation of material condition, including operating parameters of equipment in-service.The inspectors selected the following equipment trains to assess operability and properequipment line-up for a total of four samples:*11 emergency diesel generator (EDG) air start system during plannedmaintenance of the 12 EDG;*Division I electrical equipment alignment with 'B' standby gas treatment (SBGT)system out-of-service for planned maintenance;*14 emergency service water (ESW) system during 13 ESW flow test; and
- 12 core spray system with 11 core spray system out-of-service for plannedmaintenance.
b. Findings
No findings of significance were identified..2Complete System Walkdown
a. Inspection Scope
The inspectors performed a complete walkdown of equipment for one system that isimportant to safety. The inspectors walked down the system to review mechanical and electrical equipment line-ups, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of past and outstanding work orders (WOs) was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the corrective action program (CAP) database to ensure that any system equipment alignment problems were being identified and appropriately resolved.The inspectors selected the following system to assess operability and properequipment line-up for a total of one sample:*alternate nitrogen system.
b. Findings
No findings of significance were identified.
51R05Fire Protection (71111.05)Quarterly Fire Zone Walkdowns (71111.05Q)
a. Inspection Scope
The inspectors walked down risk significant fire areas to assess fire protectionrequirements. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems or features. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events, or the potential to impact equipment which could initiate or mitigate a plant transient. The inspection activities included the control of transient combustibles and ignition sources, fire detection equipment, manual suppression capabilities, passive suppression capabilities, automatic suppression capabilities, compensatory measures, and barriers to fire propagation.The inspectors selected the following areas for review for a total of seven samples:
- Fire Zone 14-A, upper 4 kV bus area (12, 14, and 16);*Fire Zone 15-A, No. 12 diesel generator room;
- Fire Zone 15-B, No. 11 diesel generator room and day tank rooms;
- Fire Zone 5-C, fuel pool skimmer tank room;
- Fire Zone 21-D, radwaste building;
- Fire Zone 27, off-gas storage building; and
- Fire Zone 37, transformers.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures (71111.06)
a. Inspection Scope
The inspectors performed an annual review of flood protection barriers and proceduresfor coping with internal flooding. The inspection focused on evaluating the licensee's preparations to mitigate flooding in the turbine building 911' and 931' elevations. The inspection activities included a review and/or walkdown of accessible areas of the turbine building.The inspectors selected the following equipment for a total of one sample:
- 4160 Vac essential switchgear rooms.
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b. Findings
No findings of significance were identified.
1R08 Inservice Inspection (ISI) Activities (71111.08)Piping Systems ISI
a. Inspection Scope
In the apparent cause evaluation (ACE) for CAP 01088981, the licensee evaluated thereasons why an ultrasonic test (UT) performed on a section of safety-related service water piping failed to detect a piping defect. The inspectors reviewed the ACE documented for CAP 01088981, which reviewed actions taken in response to a through-wall leak discovered on April 19, 2007, on a four inch diameter section of safety-related ASME Code Class 3 carbon steel pipe.This inspection activity did not constitute an inspection sample.b.FindingsUse of Unqualified Procedures for Detection of PittingIntroduction: The inspectors identified a non-cited violation (NCV) of 10 CFR 50Appendix B, Criterion IX for the licensee's failure to use a nondestructive examination (NDE) procedure qualified in accordance with Codes and Standards for detection of pitting in safety-related service water systems. Specifically, the UTs were conducted by the licensee in accordance with UT Procedure PEI-02.03.12 "Ultrasonic Detection of Pitting" which was not qualified for detection of discontinuities in accordance with ASME Section V, "Nondestructive Examination."Description: On August 22, 2007, the inspectors determined that the licensee failed touse a qualified procedure to detect pitting in safety-related service water systems.The ACE for CAP 01088981 evaluated the reasons why an UT performed on a sectionof safety-related service water piping failed to detect a through-wall piping defect. On April 19, 2007, the licensee performed informational UT of pipe segment E7 downstream of the 13 ESW pump in accordance with Procedure PEI-02.03.12
"Ultrasonic Detection of Pitting." On April 22, 2007, during post-replacement pressure testing, a through-wall leak was discovered on piping segment E7. Upon reinspection of the leaking area, the licensee determined that this flaw was "virtually undetectable using traditional UT methods." Specifically, the licensee concluded that "traditional UT examination techniques used to measure thickness were unable to identify the degraded condition related to the second leak" and that "a high gain method was required to adequately characterize the degradation."On August 22, 2007, the inspectors identified that the licensee had failed to use aqualified UT procedure for detection of pitting. The expected degradation mechanism of the ESW piping and in particular the leaking section was microbiological influenced 7corrosion (MIC). Because MIC degradation initiates at the inner surface of the pipe andtypically is cone shaped with the base larger at the inner surface and progresses to a point as it corrodes through the pipe wall, the UT procedure must be designed to detect this pitting type of degradation.During review of Procedure PEI-02.03.12, the inspectors identified that the procedurewas developed and based on ASTM E-797, "Standard Practice for Thickness Measurement by Manual Contact Ultrasonic Method." This method provides the guidelines for determining the thicknesses of materials. Because the calibration techniques established in Step 10.2 of PEI-02.03.12 were set up to meet this standard, they were not consistent with applicable Code methods used to detect pitting.
Specifically, the ASME Code,Section V, Article 23, SE-213 "Standard Practice for Ultrasonic Inspection of Metal Pipe and Tubing," states that the purpose of this practice is to outline a procedure for detecting and locating significant discontinuities such as pits, voids, inclusions, or cracks. This standard identified calibration based on reference notches and establishment of a rejection level based on these notches. The inspectors concluded that the licensee failed to incorporate appropriate Code UT standards for detection of pitting into PEI-02.03.12, which made this procedure ineffective for detection of MIC corrosion.On August 28, 2007, the licensee entered this issue into their corrective action program(CAP 01109115).Analysis: The inspectors determined that the failure of the licensee to use an adequateNDE procedure for detection and sizing of pitting (MIC) in safety-related service water systems was a performance deficiency that warranted a significance evaluation. Absent NRC intervention, the licensee's continued use and reliance on an unqualified UT procedure could place the ESW at increased risk for through-wall leakage and/or pipe failure. Therefore, this finding was of more than minor significance because it was associated with the Mitigating System cornerstone attribute of procedure quality and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems (e.g. ESW) that respond to initiating events. The inspectors determined that, in part, the cause of the performance deficiency affected the cross-cutting area of Human Performance, had resources components, and involved aspects associated with maintaining long-term plant safety by the maintenance of design margins and the minimization of long-standing equipment issues. H.2(a)]The inspectors applied the Inspection Manual Chapter (IMC) 0609, Appendix A,"Significance Determination of Reactor Inspection Findings for At-Power Situations" to this finding. Under Column 2 of the Phase 1 worksheet "Mitigating Systems Cornerstone," the inspectors answered: "No" to question 1 related to design or qualification deficiencies; "No" to questions 2, 3 and 4 related to loss of train or system safety functions; and "No" to question 5 related to seismic, flooding and severe weather.
Therefore, the finding was considered to be of very low safety significance.
Enforcement:
Title 10 CFR 50 Appendix B, Criterion IX "Control of Special Processes,"required, in part, that nondestructive testing be controlled and accomplished using qualified procedures in accordance with applicable codes, standards, specifications,criteria, and other special requirements.
8The ASME Code,Section V, Article 23, SE-213 "Standard Practice for UltrasonicInspection of Metal Pipe and Tubing," states that the purpose of this practice is to outline a procedure for detecting and locating significant discontinuities such as pits, voids, inclusions, cracks, splits by the ultrasonic pulse-reflection method.Section 8.2 of SE-213 states, in part, that longitudinal (axial) reference notches shall beintroduced on the outer and inner surfaces of the standard.Section 9 of SE-213 states, in part, that using the calibration standard specified inSection 8, adjust the equipment to produce clearly identifiable indications from both theinner and outer notches.Section 11.1 of SE-213 states, in part, that all indications that are equal to or greaterthan the rejection level established during calibration as described in Section 9 shall be considered as representative of defects and may be cause for rejection of the pipe or tube.Contrary to the above, as of August 22, 2007, the licensee had not established anNDE procedure qualified for detection of pitting in accordance with applicable Codes and Standards. Specifically, Procedure PEI-02.03.12 "Ultrasonic Detection of Pitting,"
used for detection of pitting in the ESW piping system did not specify a calibration standard with axial reference notches, did not adjust equipment to produce identifiable indications from these notches, and did not establish a rejection level based on these notches as specified by SE-213. Failure to use a qualified NDE procedure appropriate to the circumstance is a violation of 10 CFR 50 Appendix B, Criterion IX. Because of the very low safety significance of this finding and because the issue was entered into the licensee's corrective action program, it is being treated as a NCV, consistent with Section VI.A.1 of the Enforcement Policy. (NCV 05000263/2007004-01)1R11Licensed Operator Requalification Program (71111.11)
a. Inspection Scope
The inspectors performed a quarterly review of licensed operator requalification training. The inspection assessed the licensee's effectiveness in implementing the requalification program; whether licensed individuals could demonstrate operation of the facility safely and within the conditions of their license; and licensed operator performance of high-risk operator actions.The inspectors observed the following requalification activity for a total of one sample:
- a training crew during an evaluated simulator scenario that included a loss of allhigh pressure injection and a recirculation line break. This resulted in entry into emergency operating procedures, reduced reactor level control and reactor pressure blow-down.
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b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
a. Inspection Scope
The inspectors reviewed systems to assess maintenance effectiveness, includingmaintenance rule activities, work practices, and common cause issues. Inspection activities included the licensee's categorization of specific issues including evaluation of performance criteria, appropriate work practices, identification of common cause errors, extent of condition, and trending of key parameters. Additionally, the inspectors reviewed implementation of the Maintenance Rule (10 CFR 50.65) requirements, including a review of scoping, goal-setting, performance monitoring, short-term and long-term corrective actions, functional failure determinations associated with reviewed CAP documents, and current equipment performance status.The inspectors performed the following maintenance effectiveness reviews for a total oftwo samples:a function-oriented review of the residual heat removal service water (RHRSW)system motor cooler line check valves; andan issue/problem-oriented review of the 13 and 14 ESW systems due to variousflow margin issues identified over the past six months.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
a. Inspection Scope
The inspectors reviewed maintenance activities to review risk assessments (RAs) andemergent work control. The inspectors verified the performance and adequacy of RAs, management of resultant risk, entry into the appropriate licensee-established risk bands, and the effective planning and control of emergent work activities. The inspection activities included a verification that licensee RA procedures were followed and performed appropriately for routine and emergent maintenance, that RAs for the scope of work performed were accurate and complete, that necessary actions were taken to minimize the probability of initiating events, and that activities to ensure that the functionality of Mitigating Systems and barriers were performed. Reviews also assessed the licensee's evaluation of plant risk, risk management, scheduling, configuration control, and coordination with other scheduled risk significant work for these activities. Additionally, the assessment included an evaluation of external factors, the licensee's control of work activities, and appropriate consideration of baseline and cumulative risk.
10The inspectors observed maintenance or planning for the following activities or risksignificant systems undergoing scheduled or emergent maintenance for a total of five samples:*initial corrective actions taken to address low ESW flow to the 'A' residual heatremoval (RHR) room which resulted in 11 core spray pump and 13 RHR pump to be inoperable and Technical Specification (TS) 3.0.3 being entered;*emergent work to resolve extended low ESW flow to 13 RHR pump motorcooler;*troubleshooting and evaluation of flow blockage in EDG fire system deluge;
- investigation and corrective actions following a stuck-closed drain valve on the12 low pressure feedwater heater; and*work management following an increase in overall plant risk during orange gridrisk conditions on September 18, 2007.
b. Findings
Introduction:
A finding of very low safety significance was self-revealed when the12B low pressure feedwater heater drain valve unexpectedly closed causing a feedwater temperature perturbation. No violation of NRC requirements was identified.Description: On August 22, 2007, after performing a pre-job brief, instrumentmaintenance technicians commenced WO 0157987, "Perform major PM on CV-2207."
This work, associated with the 'B' condensate demineralizer, involved rebuilding the valve actuator and calibrating the positioner using plant instrument air. The technicians attached their equipment to an unlabeled instrument air quick disconnect on a local instrument rack containing several feedwater heater dump and drain valve controllers.
The particular disconnect used was located between the electric-to-pneumatic controller and valve positioner for the 12B low pressure feedwater heater drain valve (CV-1052).
Once air flow was issued by the technicians, local air pressure in the system reduced to a point where CV-1052 fully closed - with the overall result of reactor thermal power reducing by approximately one megawatt.A few moments after the feedwater perturbation occurred, the cause was quicklydetermined and WO 0157987 was halted. Troubleshooting then commenced to re-establish the appropriate air pressure and control to CV-2207.Analysis: The inspectors determined that the failure to appropriately label plantequipment that, if used could initiate a plant transient, was a performance deficiency warranting a significance evaluation in accordance with IMC 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Disposition Screening." The inspectors determined that the finding was more than minor because it involved the configuration control attribute of the Initiating Events cornerstone objective of limiting the likelihood of events that upset plant stability during power operations.The licensee determined that the primary contributing cause of the event was the lack oflabeling of the instrument air connection points. Although WO 0157987 did not contain specific information for the correct instrument air disconnect(s) to use, or caution the individuals to ensure that an instrument air header tap was used, the technicians should 11have realized the impact of attaching the test equipment. However, the licenseedetermined that the lack of labeling of the connection points was a basic hardened barrier to prevent human error that should have been in place to preclude use of the disconnect. The inspectors determined that the performance deficiency affected the cross-cutting area of Human Performance, having resource components, and involving aspects associated with the failure to correctly label plant components. H.2(c)]The inspectors evaluated the finding using IMC 0609, Appendix A, Attachment 1,"Significance Determination of Reactor Inspection Findings for At-Power Situations." Using the Phase 1 worksheet for the Initiating Events cornerstone, the inspectors determined that the finding was of very low safety significance (Green) because it was not: (1) associated with the likelihood of initiating a loss of coolant accident; (2) did not contribute to both the likelihood of a scram and unavailability of Mitigating Systems; and (3) was not associated with a fire or flood.Enforcement: The inspectors concluded that no violation of NRC requirementsoccurred. The licensee entered this finding into their corrective action program (CAP 01108192) and took immediate actions, such as implementing additional requirements for further instrument air use in the plant and a longer term action to label all available instrument air connection points at the facility.
(Finding (FIN)05000263/2007004-02).
1R15 Operability Evaluations (71111.15)
a. Inspection Scope
The inspectors reviewed operability evaluations which affected Mitigating Systems orbarrier integrity to ensure that operability was properly justified and that the component or system remained available. The inspection activities included a review of the technical adequacy of the operability evaluations to determine the impact on TS, the significance of the evaluations to ensure that adequate justifications were documented, and that risk was appropriately assessed.The inspectors reviewed the following operability evaluations for a total of five samples:
- CAP 01099800; rag sucked into duct during performance of4048 post-maintenance (PM);*CAP 01100115; low 'A' RHR room ESW flow;
- CAP 01093320; unable to locate document on control room ventilation heat loadeffect ESW system; and*CAP 01106816; charcoal filter iodine calculations non-conservative.
b. Findings
No findings of significance were identified.
121R19Post-Maintenance Testing (71111.19)
a. Inspection Scope
The inspectors verified that the PM test procedures and activities were adequate toensure system operability and functional capability. Activities were selected based upon the structure, system, or component's ability to impact risk. The inspection activities included witnessing or reviewing the integration of testing activities, applicability of acceptance criteria, test equipment calibration and control, procedural use and compliance, control of temporary modifications or jumpers required for test performance, documentation of test data, system restoration, and evaluation of test data. Also, the inspectors verified that maintenance and PM testing activities adequately ensured that the equipment met the licensing basis, TS, and USAR design requirements. The inspectors selected the following PM activities for review for a total of six samples:
- standby liquid control (SBLC) system test following the replacement of XP-12-1[RV-11-39A drain to drain tank] and XP-12-2 [RV-11-39B drain to drain tank];*12 reactor water cleanup (RWCU) system valve testing and restoration followingreplacement of filter/demineralizer isolation valves RC-41-2 and RC-88-2;*11/12 EDG fire system testing following replacement of deluge system batteries;
- 'B' SBGT system testing following planned maintenance;
- 'A' RHRSW quarterly pump and valve test following planned maintenance; and
- 11 core spray torus suction valve MO-1741 testing following electrical andmechanical maintenance.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing (71111.22)
a. Inspection Scope
The inspectors reviewed surveillance testing activities to assess operational readinessand to ensure that risk-significant structures, systems, and components were capable of performing their intended safety function. Activities were selected based upon risk significance and the potential risk impact from an unidentified deficiency or performance degradation that a system, structure, or component could impose on the unit if the condition was left unresolved. The inspection activities included a review for preconditioning, integration of testing activities, applicability of acceptance criteria, test equipment calibration and control, procedural use, control of temporary modifications or jumpers required for test performance, documentation of test data, TS applicability, impact of testing relative to performance indicator (PI) reporting, and evaluation of test data.
13The inspectors selected the following surveillance testing activities for review for a totalof five samples:*13 ESW quarterly pump tests (routine);*Reactor recirculation loop differential pressure interlock functional test (routine);
- 14 ESW comprehensive pump and valve tests (inservice test);
- 11 core spray quarterly pump and valve test (routine); and
- Average power range monitor flow referenced scram functional test (routine).
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications (71111.23)
a. Inspection Scope
The inspectors reviewed a temporary modification associated with alarm circuitry for thehigh pressure core injection (HPCI) exhaust drain pot high level instrument. The modification was performed to reduce distractions to the operators until the root cause could be corrected during the next HPCI maintenance outage. The inspectors assessed the impact of the modification on the safety function of the associated system and reviewed design documents, safety screening documents, USAR, and applicable TS.
These reviews allowed the inspectors to determine whether the temporary modification was consistent with modification documents, drawings and procedures. The inspectors also reviewed the post-installation test results to confirm that tests were satisfactory and the actual impact of the temporary modification on the permanent system and interfacing systems were adequately verified.This temporary modification review constituted one inspection sample.
b. Findings
No findings of significance were identified.2OS3Radiation Monitoring Instrumentation and Protective Equipment (71121.03).1
Inspection Planning
a. Inspection Scope
The inspectors reviewed the Monticello Nuclear Generating Plant USAR to identifyapplicable radiation monitors associated with measuring transient high and very highradiation areas including those used in remote emergency assessment. The inspectors identified the types of portable radiation detection instrumentation used for job coverage of high radiation area work, including instruments used for fixed area radiation monitorsused to provide radiological information in various plant areas, and continuous air monitors used to assess airborne radiological conditions and work areas with the 14potential for workers to receive a 50 millirem or greater committed effective doseequivalent (CEDE). In addition, the inspectors verified contamination monitors, whole body counters, and those radiation detection instruments utilized for the release of personnel and equipment from the radiologically controlled area.This review represented one inspection sample.
b. Findings
No findings of significance were identified..2Walkdowns of Radiation Monitoring Instrumentation
a. Inspection Scope
The inspectors conducted walkdowns of selected area radiation monitors (ARMs)in the radiologically controlled area to verify that they were located as described in the USAR and were adequately positioned relative to the potential source(s) of radiation they were intended to monitor. Walkdowns were also conducted of those areas where portable survey instruments were calibrated/repaired and maintained for radiation protection (RP) staff use to determine if those instruments designated "ready for use" were sufficient in number to support the RP program, had current calibration stickers, were operable, and were in adequate physical condition. Additionally, the inspectors observed the licensee's instrument calibration units and the radiation sources used for instrument checks to assess their material condition and discussed their use with RP staff to determine if they were used appropriately. Licensee personnel demonstrated the methods for performing source checks of portable survey instruments and for source checking personnel contamination and portal monitors used at the egress from the radiologically controlled area.This review represented one inspection sample.
b. Findings
No findings of significance were identified..3Calibration and Testing of Radiation Monitoring Instrumentationa.Inspection ScopePortable survey instrument calibrations were performed at the facility by RP personnel. The inspectors interviewed involved RP personnel to determine if the methods for calibration and source checks of portable survey instruments were consistent with procedures. The inspectors observed personnel performing source checks of selected survey instruments, personnel contamination monitors, and the Fastscan whole body counting system to access its adequacy. The inspectors reviewed records of calibration, operability, and alarm set points of selected process radiation monitors and personnel monitoring devices. This review included, but was not limited to the following:
15*fuel pool radiation monitors;*spent fuel pool and reactor building exhaust plenum monitor calibration records;
- certificate of calibration for small article monitors;
- certificate of calibration for Eberline radiation detection device model RM-14s;
- Fastscan whole body counter calibration;
- main steam line radiation monitor test and calibration;
- off-gas pretreatment monitor calibration; and
- control room air intake monitor calibration.The inspectors evaluated those actions that would be taken when, during calibrationor source checks, an instrument was found to be out of calibration by more than 50 percent. Those actions included an investigation of the instrument's previous usages and the possible consequences of that usage since the last calibration or source check.
The inspectors also reviewed the licensee's 10 CFR Part 61 source term analyses to determine if the calibration sources used were representative of the plant source term.This review represented one inspection sample.
b. Findings
No findings of significance were identified..4Problem Identification and Resolution
a. Inspection Scope
The inspectors reviewed the licensee's self-assessments, audits, and corrective actiondocuments that involved personnel contamination monitor alarms due to personnel internal exposures to determine if identified problems were entered into the CAP for resolution. There were no internal exposure occurrences greater than 50 millirem CEDE that were evaluated during the inspection. However, the licensee's process for investigating this type of occurrence was reviewed to determine if the affected personnel would be properly monitored utilizing the appropriate equipment and if the data would be analyzed and internal exposures properly assessed in accordance with licensee procedures.The inspectors reviewed CAP reports related to exposure of workers or to significantradiological incidents that involved radiation monitoring instrument deficiencies since thelast inspection in this area. Staff members were interviewed and corrective action documents were reviewed to determine if follow-up activities were being conducted in an effective and timely manner commensurate with its importance to safety and risk-based on the following:*initial problem identification, characterization, and tracking;*disposition of operability/reportability issues;
- evaluation of safety significance/risk and priority for resolution;
- identification of repetitive problems;
- identification of contributing causes; 16*identification and implementation of effective corrective actions;*resolution of NCVs tracked in the corrective action system; and
- implementation/consideration of risk significant operational experience feedback. The inspectors evaluated the licensee's self-assessment activities to determine if theywould identify and address repetitive deficiencies or significant individual deficiencies observed in problem identification and resolution.These reviews represented three inspection samples.
b. Findings
No findings of significance were identified..5RP Technician Instrument Use
a. Inspection Scope
The inspectors determined if the calibration expiration and source response check datarecords on radiation detection instruments staged for use were current and observed RP technicians for appropriate instrument selection and self-verification of instrument operability prior to use.This review represented one inspection sample.
b. Findings
No findings of significance were identified..6Self-Contained Breathing Apparatus (SCBA) Maintenance/Inspection and User Training
a. Inspection Scope
The inspectors reviewed the status, maintenance and surveillance records of selectedSCBAs staged and ready for use in the plant and assessed the licensee's capability for refilling and transporting SCBA air bottles to and from the control room during emergency conditions. The inspectors determined whether control room operators and other emergency response and RP personnel were trained and qualified in the use of SCBA, including personal bottle change-out. The inspectors also reviewed the training and qualification records for selected individuals on each control room shift crew and selected individuals from each designated department that were currently assigned emergency duties, including on-site search and rescue, to determine if an adequate number of personnel were qualified for emergency response activities.The inspectors reviewed the SCBA manufacturer's maintenance training certificationsfor licensee personnel qualified to perform SCBA maintenance on vital components (regulator and low pressure alarm). The inspectors reviewed maintenance records for several SCBAs designated as "ready for service." The inspectors verified that 17maintenance was performed by qualified personnel over the past five years. Theinspectors also determined if the required periodic air cylinder hydrostatic testing was current and documented. The inspectors also evaluated if the licensee's maintenance procedures were consistent with the SCBA manufacturer's maintenance manuals.These reviews represented two inspection samples.
b. Findings
No findings of significance were identified.4.OTHER ACTIVITIES4OA1Performance Indicator Verification (71151)Cornerstones: Mitigating Systems, and Barrier Integrity.1Reactor Safety Strategic Area
a. Inspection Scope
Cornerstone: Mitigating SystemsThe inspectors' review of PIs used guidance and definitions contained in Nuclear EnergyInstitute (NEI) Document 99-02, Revision 5, "Regulatory Assessment Performance Indicator Guideline," to assess the accuracy of the PI data. The inspectors reviewed licensee event reports (LERs), data within operator logs, Mitigating Systems Performance Index (MSPI) derivation reports, and CAP documents for each PI.The following PIs were reviewed for a total of three samples:*MSPI for Emergency Alternating Current Power System, for the period ofJuly 2006 through June 2007;*MSPI for High Pressure Injection System, for the period of July 2006 throughJune 2007; and*MSPI for Heat Removal System, for the period of July 2006 through June 2007.
b. Findings
No findings of significance were identified.
18Cornerstone: Barrier Integrity
a. Inspection Scope
The inspectors sampled the licensee's PI submittals for the periods listed below. Theinspectors used PI definitions and guidance contained in Revision 5 of NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," to verify the accuracy of the PI data. The following PI was reviewed:*Reactor Coolant System Specific Activity.
The inspectors reviewed chemistry department records and selected isotopic analysesfrom January 2006 through June 2007 to determine if the greatest dose equivalent iodine (DEI) values obtained during those months corresponded with the values reported to the NRC. The inspectors also reviewed selected DEI calculations to verify that the appropriate conversion factors were used in the assessment. Additionally, the inspectors observed a chemistry technician obtain and analyze a reactor coolant sample for DEI to determine if there was adherence with licensee procedures for the collection and analysis of reactor coolant system samples.This review represented one inspection sample.
b. Findings
No findings of significance were identified.4OA2Identification and Resolution of Problems (71152)Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, andEmergency Preparedness.1Routine Review of Identification and Resolution of Problems
a. Inspection Scope
As part of the routine inspections documented above, the inspectors verified that thelicensee entered the problems identified during the inspection into their CAP.
Additionally, the inspectors verified that the licensee was identifying issues at an appropriate threshold and entering them in the CAP, and verified that problems included in the licensee's CAP were properly addressed for resolution. Attributes reviewed included: complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrence reviews were proper and adequate; and that the classification, prioritization and focus were commensurate with safety and sufficient to prevent recurrence of the issue.
19
b. Findings
No findings of significance were identified..2Daily Corrective Action Program Reviews
a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specifichuman performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished by reviewing daily CAP summary reports and attending corrective action review board meetings.
b. Findings
No findings of significance were identified.4OA3Event Follow-up (71153).1(Closed) Licensee Event Reports 50-263/2007-003-00 and 50-263/2007-003-01: "Failure to Enter a Required Technical Specification Action During Control Rod Drive Exercising"On April 20, 2007, with the plant in Mode 4, the licensee performed control rodexercising. While exercising Control Rod 26-31, the operators realized that they did not get the same back light indication for the control rod that they had received for the previously tested rod (26-35). The incorrect back light indication meant that the one rod out interlock for Control Rod 26-35 was inoperable. The one rod out interlock for Control Rod 26-35 should have been declared inoperable and the appropriate TS actions should have been taken prior to commencing testing on Control Rod 26-31.
The licensee determined that the cause of this event was incorrect acceptance criteria in the procedure being used to perform the testing, and that lack of operator proficiency and misdiagnosis of the indications were contributing causes. Corrective actions taken by the licensee to address this issue included: replacing the defective control rod position indication probe; improving the testing procedure; and providing additional training to their operating crews.During their review of the original submittal of this LER, the inspectors challenged thelicensee's report in two areas. The first area was the licensee's conclusion that the failure of control rod position indicator probe for Control Rod 26-35, and subsequent inoperability of the refuel position one-rod-out interlock, was not a safety system functional failure. The second area that the inspectors challenged was the quality of the evaluations documented in the LER's safety significance section. Specifically, the narrative in this section discussed, in part, that the one-rod-out interlock is designed to ensure that movement of more than one control rod is restricted to prevent the reactor from becoming critical during refueling operations. Additionally, the narrative stated that at no time were Control Rods 26-35 and 26-31 both fully withdrawn at the same time, that at no time did the reactor become critical during the control rod exercising, and that 20no fuel damage would have occurred even if both rods had been fully withdrawn. Theinspectors noted that the licensee's safety significance evaluation did not discuss whether or not reactor criticality was possible if Control Rods 26-35 and 26-31 had both been fully withdrawn and what other barriers, minus the one-rod-out interlock, were in place that would have mitigated or prevented an inadvertent shutdown criticality event.In response to the inspectors' questions, the licensee submitted Revision 1 toLER 50-263/2007-003. After further evaluation of the issue, the licensee determined that failure of control rod position indicator probe for Control Rod 26-35, and subsequent inoperability of the refuel position one-rod-out interlock, was a safety system functional failure. Additionally, the licensee enhanced their safety significance evaluation to discuss the potential impact of a shutdown criticality event associated with this issue and the additional barriers that were in place that prevented its occurrence.The performance deficiency associated with the failure to enter a TS during control rodtesting was previously evaluated and determined to be a licensee-identified finding of very low safety significance and is documented in Section
4OA7 of Inspection Report
(IR) 05000263/2007003. The inspectors concluded that the licensee's failure to identify the safety system functional failure associated with the failure of control rod position indicator probe for Control Rod 26-35, and subsequent inoperability of the refuel position one-rod-out interlock, was a finding of minor significance because it would not have caused the licensee to challenge the White Safety System Functional Failure Performance Indicator threshold for the second quarter of 2007. This original LER, and subsequent Revision 1 are closed..2(Closed) Licensee Event Report 50-263/2007-004-00: "Degradation of EmergencyService Water Flow to Emergency Core Cooling System Room Cooler"On July 2, 2007, the licensee notified the NRC via LER 50-263/2007-004-00 that a lowflow condition for the 'A' RHR room components existed during a 13 ESW quarterly pump and valve test. Technical Specification 3.5.1 Conditions 'A,' 'B,' and 'M' were entered, resulting in immediate entry into TS 3.0.3 - a one-hour shutdown statement.
The 'A' RHR room ESW piping was immediately flushed and TS 3.5.1 Conditions 'B' and 'M,' and TS 3.0.3 were exited before power reduction commenced. The 13 RHR pump remained inoperable via TS 3.5.1 condition 'A,' a 30-day action statement, due to not having direct flow rate measurement to the motor cooler. The licensee later determined the causes of the low flow condition were attributed to throttling of the 'A' RHR room cooler ESW outlet valve during the recent refueling outage resulting in silt accumulation at the valve and inadequate testing methodology and acceptance criteria.
The licensee determined that ESW flow had fallen below required values on or about May 25, 2007. Corrective actions included performance of a calculation to determine and clarify appropriate acceptance criteria, and initiation of a long term improvement project to resolve flow margin issues. The inspectors determined that a performance deficiency existed in that the licensee did not adequately evaluate and control the change in configuration to the system when the room cooler outlet valve was throttled.
This finding is more than minor because it affected the equipment performance attribute of the Mitigating Systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable 21consequences. Specifically, continued operation of all Division I low pressureemergency core cooling systems (ECCSs) would have been challenged during a real event with reduced cooling flow. The finding was considered to have very low safety significance (Green) because the licensee demonstrated the ability to flush the system in accordance with station procedures in an expedited manner; loss of cooling water was assumed to not have an impact on the operation of the pumps for at least 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and redundant systems were available throughout the period of the low flow conditions.
Although both trains of the decay heat removal and containment cooling safety functions were considered inoperable for a few hours during RHRSW pump replacement between the dates of May 25 and July 2, 2007, the exposure time was minimal. The licensee-identified finding involved a violation of TS 3.5.1, ECCS - Operating. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed..3(Closed) Licensee Event Report 50-263/2007-005-00: "Discovery of Appendix R -Non-Compliant Manual Actions during Review of NFPA 805"On July 12, 2007, the licensee notified the NRC via LER 50-263/2007-005-00 thatcertain manual operator actions to achieve and maintain 10 CFR 50, Appendix R, "Fire Protection Program for Nuclear Facilities Operating Prior to January 1, 1979," hot shutdown were non-compliant. This issue is discussed in detail in Section 4OA7. This LER is closed..4(Closed) Unresolved Item (URI) 05000263/2007002-04: "Operator Performance DuringDivision II RHR Logic Testing on February 7, 2007"Introduction: A finding of very low safety significance was self-revealed for a violation of10 CFR 50, Appendix B, Criterion V, when licensed operators failed to perform Procedure OSP-RHR-0545-02, "RHR Containment Spray/Cooling LogicTest-Division II,"in accordance with the written instructions of the procedure. Specifically, the licensed operators landed a test jumper in the wrong electrical cabinet during the conduct of the test. Additionally, after identifying the error, the operators took actions to remove the incorrectly landed test jumper, install the test jumper at the correct location, and proceed with the test, without first notifying management. These actions were not allowed by the test procedure, nor were they in accordance with operations department standards and expectations.Description: A complete description of the event was documented in IntegratedIR 05000263/2007002. During the time since IR 05000263/2007002 was completed, the NRC further evaluated the licensed operator performance associated with this issue and did not identify any additional findings beyond the performance deficiency documented in this section of this report.
Analysis:
The inspectors determined that the failure to perform testing on safety-relatedequipment in accordance with approved procedures was a performance deficiency warranting a significance evaluation. The inspectors concluded that the finding was greater than minor in accordance with IMC 0612, "Power Reactor Inspection Reports,"
Appendix B, "Issues Disposition Screening," issued on June 22, 2006. The finding was 22more than minor because it affected the configuration control attribute of MitigatingSystems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined that the performance deficiency affected the cross-cutting area of Human Performance, having decision making components and involving aspects associated with making safety-significant or risk-significant decisions using a systematic process, especially when faced with uncertain plant conditions, to ensure safety is maintained. H.1(a)]Utilizing the Phase 1 Screening Worksheet, per IMC 0609, "Significance DeterminationProcess," the inspectors determined that the finding was of very low safety significance because it was not associated with a design or qualification deficiency, did not result in the loss of a train or safety system function, and was not related to seismic, flooding, or severe weather event.Enforcement: Title 10 CFR 50, Appendix B, Criterion V requires, in part, that activitiesaffecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances and shall be accomplished in accordance with these procedures.
Contrary to this requirement, the licensee failed to perform Procedure OSP-RHR-0545-02, "RHR Containment Spray/Cooling Logic Test - Division II," inaccordance with the written instructions of the procedure. Because the event was of very low safety significance and because the issue was entered into the licensee's corrective action program (CAPs 01075924 and 01075923), this violation is being treated as an NCV, consistent with Section VI.A.1 of Enforcement Policy (NCV 05000263/2007004-03)..5Monticello Nuclear Generating Plant Technical Support Center (TSC) PlannedRelocation ActivitiesOn July 16, 2007, the licensee made a 50.72(b)(3) eight hour non-emergencynotification associated with the planned relocation of their existing TSC to a newly constructed facility also located within the protected area. The inspectors ensured that adequate compensatory measures were being implemented by the licensee to ensure that TSC functions were being maintained during the transition. The new TSC was declared fully functional at 14:00 on July 19, 2007..6Unanalyzed Condition Impacting Both Divisions of Essential SwitchgearOn July 26, 2007, at 09:02, the licensee made a 50.72 non-emergency notificationassociated with an unanalyzed condition which had the potential to impact both divisions of their essential switchgear. The issue, as stated in the notification, was identified when an operator noticed that a normally open fire door had closed due to the failure of a fusible link. The impact of the door being closed was that the pathway for a potential flood due to a high energy line break was blocked; therefore, closing off a drain path for the water. This unanalyzed condition had the potential to impact both divisions of essential switchgear, and as a result, both divisions of essential switchgear were declared inoperable and TS 3.0.3 was entered. At 09:55, the fire door was returned to its required open state and TS 3.0.3 was exited.
23The inspectors evaluated the licensee's initial response to the event and no findings ofsignificance were identified. This event will be further evaluated by the inspectors once the LER is completed by the licensee..7Licensee Response to Anticipated Degrading River Flow ConditionsOn August 7, 2007, the licensee observed a significant reduction in upstream river flow.Based on minimum flow procedure requirements, plant equipment river level requirements, and flow appropriation limits with the State of Minnesota, the licensee began preparations to reduce reactor power. The inspectors observed the licensee's activities associated with troubleshooting the cause of the reduced flow conditions, discussions between licensee staff to support the potential power reduction, and operations activities in monitoring river conditions.Although a power reduction was ultimately not required, the licensee demonstrated anoverall conservative approach to maintaining margin between river operating conditions and level requirements to maintain operability of plant equipment. No findings of significance were identified.4OA6Meetings.1Exit MeetingThe inspectors presented the inspection results to Mr. O'Connor and other members oflicensee management on October 4, 2007. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified..2Interim Exit MeetingsInterim exits were conducted for:
- Radiation monitoring instrumentation and protective equipment and barrierintegrity performance indicator with Mr. John Sabados, General Supervisor of Chemistry on July 13, 2007.4OA7Licensee-Identified ViolationsThe following violations of very low safety significance (Green) were identified by thelicensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.*Technical Specification 3.5.1 requires, in part, that each ECCS injection/spraysubsystem shall be operable. Contrary to this, on July 2, 2007, multiple Division I low pressure ECCS (11 and 13 RHR, 11 core spray) were not operable. Because of this condition, TS 3.5.1 Condition M would have required immediate entry into TS 3.0.3, requiring a plant shutdown to commence within 24one hour. This was not done due to the unanalyzed condition discovered by thelicensee during the 13 ESW quarterly pump and valve test. This was identified in the licensee's corrective action program as CAP 01100115. This finding is of very low safety significance because the low flow condition could be corrected in an expedited manner and no impact on the safety function would occur.*Title 10 CFR 50, Appendix R required, in part, that one of three specified meansof ensuring that one of the redundant trains was free of fire damage to achieve and maintain hot shutdown. Contrary to this requirement, the licensee failed to ensure that manual operator actions in place were in compliance with one of the three specified means of 10 CFR 50, Appendix R, Section III.G.2. The licenseereported this event to the NRC on August 30, 2007, pursuant to 10 CFR 50.73(a)(2)(ii)(B) via LER 50-263/2007-005-00.The licensee's discovery occurred during review of National Fire ProtectionAssociation (NFPA) 805, "Transition Project Task SUP-1," and Regulatory Issue Summary (RIS) 2006-10, "Regulatory Expectations with Appendix R Paragraph III.G.2 Operator Manual Actions." Based on the criteria for allowablemanual actions specified in RIS 2006-10, actions credited to limit fire damage for the fire areas housing vital 4kV electrical components were not allowed by Section III.G.2 of 10 CFR 50, Appendix R.Prior to the issuance of RIS 2006-10, the licensee considered the manualoperator actions to be acceptable based on current industry guidance. The inspectors determined that the failure to have in place compliant operator manual actions to ensure that one redundant train of systems were protected to maintain hot shutdown conditions was a performance deficiency warranting significance evaluation. The inspectors concluded that the finding was more than minor in accordance with IMC 0612, "Power Reactor Inspection Reports," Appendix B,
"Issue Screening." The finding involved the attribute of protection against external factors and could have affected the Mitigating Systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The licensee documented the unanalyzed condition in CAP 01101494, and upon discovery, performed an evaluation to determine that the effect of not performing the manual operator actions would have had a minimal effect on plant safety. The inspectors reviewed the licensee's evaluation and concluded it was appropriate.
Corrective actions included future evaluation of the non-compliant manual operator actions to either accept as-is or to conduct plant modifications. The procedure-controlled operator manual actions would remain intact as compensatory measures.Because the licensee-identified violation was not associated with a finding ofhigh safety significance, the inspectors evaluated the violation in accordance with the four criteria established by Section A of the NRC's Interim Enforcement Policy Regarding Enforcement Discretion for Certain Fire Protection Issues (10 CFR 50.48) for a licensee in NFPA 805 transition. The inspectors determined that for this violation: (1) the licensee identified the violation during 25the scheduled transition to 10 CFR 50.48(c); (2) the licensee had in placeadequate compensatory measures and would correct the violation as a result of completing the NFPA 805 transition; (3) the violation was not likely to have been previously identified by routine licensee efforts; and (4) the violation was not willful. As a result, the inspectors concluded that the violation met all four criteria established by Section A and the NRC was exercising enforcement discretion to not cite this violation in accordance with the NRC's Enforcement Policy.ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- T. O'Connor, Site Vice President
- B. Sawatzke, Plant Manager
- J. Grubb, Site Engineering Director
- W. Guldemond, Nuclear Safety Assurance Manager
- S. Sharp, Operations Manager
- S. Radebaugh, Maintenance Manager
- K. Jepson, Radiation Protection/Chemistry Manager
- R. Baumer, Compliance Engineering Analyst
- J. Sabados, General Supervisor of Chemistry
- P. Vitalis, Radiation Protection, Health Physicist
- B. Weller, Radiation Protection Supervisor
- K. Pederson, Chemistry
- R. Nuelk, System Engineer Radiation/Process MonitorsNuclear Regulatory Commission
- K. Riemer, Chief, Reactor Projects Branch 2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and
Closed
- 05000263/FIN-2007004-01NCVUnqualified Procedure for Detection of Pitting(Section 1R08)
- 05000263/FIN-2007004-02FINFeedwater Perturbation due to Instrument Air PressureReduction to Feedwater Heater Drain Valve Positioner
(Section 1R13)
- 05000263/FIN-2007004-03NCVOperators Failed to Perform Test Procedure InAccordance With Procedure (Section 4OA3.4)Closed50-263/2007-003-00LERFailure to Enter a required Technical Specification ActionDuring Control Rod Drive Exercising (Section 4OA3.1)50-263/2007-003-01LERFailure to Enter a required Technical Specification ActionDuring Control Rod Drive Exercising (Section 4OA3.1)50-263/2007-004-00LERDegradation of Emergency Service Water Flow toEmergency Core Cooling System Room Cooler
(Section 4OA3.2)
- 250-263/2007-005-00LERDiscovery of Appendix R - Non-Compliant Manual Actionsduring Review of NFPA 805 (Section 4OA3.3)50-263/2007002-04 URIOperator Performance During Division II RHR LogicTesting on February 7, 2007 (Section 4OA3.4)DiscussedNone.
- Attachment3
LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection.
- Inclusion on this list doesnot imply that the NRC inspectors reviewed the documents in their entirety but rather that selected sections of portions of the documents were evaluated as part of the overall inspection effort.
- Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection reports.1R01Adverse WeatherOperations Memo 07-29; Degrading River Conditions; effective date July 16 to
- October 16, 2007.
- A.6; Acts of Nature; Revision 261R04Equipment AlignmentB.08.04.03-01; Alternate Nitrogen System Function and General Description of System;
- Revision 2
- 2154-45; Alternate Nitrogen System Prestart Valve Checklist; Revision 7
- NG-36049-10; Alternate Nitrogen Supply System Piping and Instrumentation Diagram;
- Revision P
- 2154-28; Diesel Generator Air Start System Prestart Valve Checklist; Revision 9
- B.09.08-02; EDGs - Description of Equipment; Revision 9
- 2112; Plant Prestart Checklist SBGT System; Revision 11
- 1339; ECCS Pump Motor Cooler Flush; Revision 21
- 2154-11; Core Spray System Prestart Valve Checklist; Revision 18
- 2119; Plant Prestart Checklist Core Spray System; Revision 81R05Fire ProtectionStrategy A.3-14-A; Fire Zone 14-A, Upper 4 kV Bus Area (12, 14, & 16); Revision 13Strategy A.3-15-A; Fire Zone 15-A, No. 12 Diesel Generator Room; Revision 7
- Strategy A.3-15-B; Fire Zone 15-B, No. 11 Diesel Generator Room and Day Tank Rooms;
- Revision 9
- Strategy A.3-05-C; Fire Zone 5-C, Fuel Pool Skimmer Tank Room; Revision 3
- Strategy A.3-21-D; Fire Zone 21-D, Radwaste Building; Revision 4
- Strategy A.3-27; Fire Zone 27, Off-Gas Storage Building; Revision 3
- Strategy A.3-37; Fire Zone 37, Transformers; Revision 51R06Flood Protection MeasuresCAP
- 01103584; Door 18 Found Closed; July 26, 2007CA-07-021; Reactor Building, Turbine Building & Intake Structure Water Height - Internal Flooding; Revision 0
- DBD T.08; Design Basis Document for Internal Flooding; Revision 3
- Ops Man C.4-I; Plant Flooding; Revision 3
- 01088981; Adverse Trend:
- Monitoring Fails to Pre-Identify Pipe Wall Failures
- PEI-02.03.12 Inadequate1R11 Licensed Operator Requalification ProgramSimulator Exercise Guide
- RQ-SS-02; Loss of All High Pressure Injection with a Recirc Break
- Inside the Drywell; Revision 221R12 Maintenance EffectivenessMonticello Maintenance Rule Program System Basis Document; ESW System; Revision 14058-01-PM; RHR Pump 11, 13 and Core Spray Pump 11 Motor Cooler Chemical Cleaning;
- Revision 13
'A' RHR Room Air Cooling Unit V-AC-5 Internal Cleaning, External Cleaning and Visual Inspection; Revision 10
- 1339; ECCS Pump Motor Cooler Flush; Revision 19, 20
- 3107; Inservice Test Deviation From Criteria Control Room Supervisor's Immediate Action;
- Revision 26 for CAP 01100139
- 3108; Pump/Valve/Instrument Record of Corrective Action; Revision 13 for CAP 01100139
- 255-11-III-3; 13 ESW Quarterly Pump and Valve Tests; Revision 38OWI-02.07; Operations Work Control; Revision 19
- Monticello Station Logs for July 2-3, 2007
- FSW-I, Measure Flow to 'A' RHR Room; April 11, 2007
- 3749-02; Monticello Impact Statement; Revision 1 for WO 321749
- CAP 01108564; NRC Questions on
- SW-21-1,
- SW-21-2,
- SW-22-1, and SW-22-2
- WO 0294120 (Valve SW-22-2)
- Monticello Maintenance Rule Program System Basis Document; RHRSW System; Revision 1
- CAP 00841827; Plug on Check Valves
- SW-21-2 &
- SW-22-2 Were Found Frozen in Closed Position
- CAP 01106154;
- SW-22-2 Check Valve Found Stuck in the Open Position
- CAP 01013966; Change Frequency of
- SW-21-1,
- SW-22-1,
- SW-21-2, SW-22-2
- AWI-09.04.01; Inservice Testing Program; Revision 29
- WO 294120; Perform Post-Maintenance for SW-22-2
- WO 157987-01; Rebuild Actuator and Calibrate Positioner
- WO 157987-03; Restore 12B Heater Level Control to LC-1052
- 3749; Monticello Impact Statement for WO 157987
- 263; Maintenance and Construction Pre-Job Briefing Checklist; Revision 171R13 Maintenance Risk Assessments and Emergent Work Control0255-11-III-3; 13 ESW Quarterly Pump and Valve Tests; Revision 38; dated July 7,
- 20073107; Inservice Test Deviation From Criteria, Control Room Supervisor's Immediate Action;
- ESW Reference Flow Below 141-145 gpm Flow Attachment51339; ECCS Pump Motor Cooler Flush; Revision 20; dated July 2, 2007CAP
- CAP 01100139; ESW Header Flow Low During 0255-11-III-3 TestingCA-07-045; RHR Pump Model 5K511DT5410 Cooling Coil Minimum Flow Evaluation Monitoring Plan for ESW Flow Within the Reactor Building
- 8039; RHR Motor Replacement,
- EC 11169; Revision 0
- CAP 01106280; FME:
- EDG Deluge Seat Missing Rubber
- WO 341476-07; Flush/Inspect 11 Diesel Generator Room and Day Tank Rooms Deluge Systems
- 24; Fire Protection System - Sprinkler System Tests; Revision 341R15Operability EvaluationsCAP
- 01093320; Unable to Locate Document on Control Room Ventilation Heat Load Effect
- ESW System
- OSP-EFT-0557; Control Room Ventilation Heat Load Removal Test; Revision 0
- 255-11-III-7; 13 ESW Comprehensive Pump and Valve Test; Revision 10
- C.6-274A-A-06; Low Condenser Water Flow; Revision 4
- C.6-242-A-01; V-EAC-14A Low Flow; Revision 3
- CAP 01106816; Charcoal Filter Iodine Loading Calculations Non-Conservative1R19Post-Maintenance Testing0255-02-III; SBLC Quarterly Pump and Valve Test; Revision 43; dated June 28, 2007 and
- July 10, 2007
- 00323258;
- XP-12-2, Replace Valve
- RC-41-2, Remove Old Valve and Weld in a New Valve
- RC-88-2, Remove Old Valve and Weld in a New Valve
- 3069; Post-Maintenance Testing Activities Control Cover Sheet; Revision 13 for WOs 333073
and 333074
- B.02.02-05; RWCU - System Operation; Revision 31
- CAP 01105540; Actuation of Fire System During Battery Replacement of C-371
- CAP 01105603; Electric Fire Pump Did Not Start When Alarm 20-A-36 Received
- CAP 01106280; FME:
- EDG Deluge Seat Missing Rubber
- 253-02; SBGT 'B' Train Testing; Revision 34
- 0147-02; 'B' Train Standby Gas Treatment System Filter Tests; Revision 32
- CAP 01110281;
- VC-1728, Valve fails to meet IST Requirements
- CV-1728, Repack Valve and Perform Diagnostic Testing
- 255-05-IA-1-1; 'A' RHRSW Quarterly Pump and Valve Test; Revision 60
- Attachment63108; Pump/Valve/Instrument Record of Corrective Action for
- WO 3172323107; Inservice Test Deviation From Criteria Control Room Supervisor's Immediate Action for
- CAP 01110281
- MO-1741, 4900-02-PM
- 4900-02-PM; Rotork Motor Operated Valves - Inspection and Maintenance; Revision 19
- 4901-04-PM; Torque Switch Adjustment Procedure for Rotork Valve Operators; Revision 71R22Surveillance Testing0255-11-III-3; ESW Quarterly Pump TestsCAP
- 01107230;
- DPIS-2-129D Recirc Loops
- DP-Low Pressure Coolant Injection Sel Intlk Reset Problems
- ISP-RHR-0522-01; Reactor Recirculation Loops DP Low Pressure Coolant Injection Select Interlock Channel Functional Test; Revision 0
- 0012; Average Power Range Monitor/Rod Block Scram Surveillance Check; Revision 41
- CAP 01077469;
- DPIS-2-129D (RECIRC LOOP DP) Failed to Reset During Testing
- 255-11-III-8; 14 ESW Comprehensive Pump and Valve Tests; Revision 130255-03-IA-1-1; Core Spray Loop 'A' Quarterly Pump and Valve Tests; Revision 46
- CAP 1111832; Unable to Perform IST Step in Quarterly Core Spray Test1R23Temporary Plant ModificationsEngineering Change 10943 and 50.59 Screening 07-0318; Modified Alarm for
- ANN-3-B-2 High Pressure Coolant Injection Exhaust Drain Pot High Level; Revision 02PS2Radiation Monitoring Instrumentation and Protective EquipmentUSAR; Revision 23AR
- 01088619; Service Water Radiation Monitor Spiked When Operations Performed Routine Weekly Flush; dated April 19, 2007
- CAP 01045399 -
- RCE 01045399-01; Recurring Inadvertent Trip of 'B' Fuel Pool Radiation Monitor Results In Repeated Partial Group II Isolation, ESP Actuation and Reportable Event
- 2007-002-5-007; Nuclear Oversight Observation Report - Periodic Reviews of Count Room and Laboratory Equipment Response Data from February 2007; dated June 12, 2007
- 2007-002-5-017; Nuclear Oversight Observation Report- Radiological Protection; dated
- June 2, 2007
- SCBA Inspection and Functional Check; Revision 19
- F550-4-995-12-2005; Calibration of Electrometer Model No. 500; and Electrometer S/N 328; by Fluke Biomedical; dated August 16, 2005
- MSA SCBA Functional Check (740L); Hydrostatic Test Records; dated July 13, 2007
- 24; Area Radiation Monitor Calibration; 1025-B Area Radiation Monitor Test; Revision 29; dated February 23, 2007
- 0461; Control Room Air Intake Monitor Calibration, Revision 13; 0461 Control Room Air Intake Radiation Monitor Calibration; and 0460-B Control Room Air Intake Radiation Monitor Monthly
- Test; dated March 17, 2007
- 0372-02; Stack Wide Range Process and Sample Flow Instrument Calibration Procedure
(Channel B); Revision 4, 0372-02 Stack Wide-Range Gas Monitor Process; and Sample Flow Calibration; dated June 4, 2007
- Attachment70071; Off-Gas Pretreatment Monitor Calibration, Revision 30; 0071 Off-Gas Pretreatment
- Monitor Calibration and 0070-B Off-Gas Pretreatment Monitor Functional Test;
dated March 25, 2007
- 0068; Spent Fuel Pool and Reactor Building Exhaust Plenum Monitor Calibration, Revision 29
- 0068 Spent Fuel Pool Monitor Calibration; 0067-B Spent Fuel Pool Monitor Functional Test
- 0439-B Reactor Building Exhaust Plenum Monitor Functional Test; 0440 Reactor Building Exhaust Plenum Monitor Calibration Test; dated June 4, 2007
- 0372-01; Stack Wide Range Gas Monitors Process and Sample Flow Instrument Calibration
Procedure
(Channel A); Revision 4; dated June 4, 2007
- 1414; Main Steam Line Radiation Monitor Test and Calibration; Revision 7;
dated February 6, 2007
- 5504; Whole Body Counter Calibration; Revision 4; dated January 29, 2007
- Technical Basis Document No.04-002; Evaluation of the Canberra Argos Zeus-4G Personnel Contamination Monitor
- R.09.07;
- RO-2/RO-2A/RO20 Checks; Revision 19
- R.09.22; Frisker Calibration and Functional Check; Revision 21; dated July 11, 2007
- R.09.65;
- DMC-2000 Electronic Dosimeter Calibration; Revision 0
- Technical Basis Document No.04-001; Revision 0; Justification For Use of the Tool Monitor in Lieu of Frisk and Smear Surveys to Free Release Eligible Items4OA1Performance Indicator VerificationDose Equivalent Iodine -131 from November 19, 2005 to July 11,
- 20070122; Reactor Coolant I-131 Dose Equivalent Activity; Revision 25; dated July 11, 2007
- I.03.39; MCA Operation/Gamma Isotopic Analysis; Revision 7
- PRA-CALC-05-003; MSPI Basis Document; Revision 1
- Emergency Alternating Current Power System MSPI Derivation Reports:
- Unavailability Index, Unreliability Index, and Performance Limit Exceeded; July 2006 through June 2007
- High Pressure Injection System MSPI Derivation Reports:
- Unavailability Index, Unreliability Index, and Performance Limit Exceeded; July 2006 through June 2007
- Heat Removal System MSPI Derivation Reports:
- Unavailability Index, Unreliability Index, and Performance Limit Exceeded; July 2006 through June 2007
- Monticello Station Logs; July 1, 2006 through June 30, 2007
- MSPI Unavailability Entry Comments for Emergency AC Power, HPCI, and Heat Removal Systems; July 2006 through June 20074OA2Identification and Resolution of ProblemsCAP
- 01104540; NRC Identified Problems with
- LER 2007-03 Following ReviewCAP
- 01104401; Possible Non-Factual Information in NRC Submittal4OA3Event Follow-upRoot Cause Evaluation (RCE)
- 01100115-02; Emergency Service Water (FSW)
LIST OF ACRONYMS
- ASM [[]]
- CA [[]]
- CED [[]]
- CF [[]]
- DE [[]]
- DR [[]]
- ECC [[]]
- ED [[]]
- ES [[]]
- FI [[]]
- HPC [[]]
- IM [[]]
CInspection Manual Chapter
- IS [[]]
IInservice Inspection
kVKilovolt
- LE [[]]
- MI [[]]
- MNG [[]]
- MSP [[]]
- NC [[]]
- ND [[]]
- NFP [[]]
- NE [[]]
- NM [[]]
- NR [[]]
- PAR [[]]
SPublicly Available Records
PIPerformance Indicator
PMPlanned, Preventative or Post-Maintenance
- RH [[]]
- RHRS [[]]
- RI [[]]
SRegulatory Issue Summary
- RWC [[]]
- SBG [[]]
- SBL [[]]
- SCB [[]]
- SD [[]]
PSignificance Determination Process
- TS [[]]
- UR [[]]
- USA [[]]
RUpdated Safety Analysis Report
UTUltrasonic or Ultrasonic Test
VacVolts Alternating Current