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{{#Wiki_filter:ENT000427
{{#Wiki_filter:UNITED STATES  
                                                                              Submitted: March 30, 2012
              NUCLEAR REGULATORY COMMISSION  
                                      UNITED STATES
                                                        REGION I  
                          NUCLEAR REGULATORY COMMISSION
                                              475 ALLENDALE ROAD  
                                            REGION I
                              KING OF PRUSSIA, PA 19406-1415  
                                        475 ALLENDALE ROAD
                                    KING OF PRUSSIA, PA 19406-1415
                                          May 14, 2009
Mr. Joseph E. Pollock
Site Vice President
Entergy Nuclear Operations, Inc.
May 14, 2009  
Indian Point Energy Center
450 Broadway, GSB
Buchanan, NY 10511-0249
Mr. Joseph E. Pollock  
SUBJECT:         INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED
Site Vice President  
                INSPECTION REPORT 05000247/2009002
Entergy Nuclear Operations, Inc.  
Dear Mr. Pollock:
Indian Point Energy Center  
On March 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
450 Broadway, GSB  
at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report
Buchanan, NY 10511-0249  
documents the inspection results, which were discussed on April 15, 2009, with you and other
members of your staff.
SUBJECT:  
The inspection examined activities conducted under your license as they relate to safety and
INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED  
compliance with the Commissions rules and regulations, and with the conditions of your
INSPECTION REPORT 05000247/2009002  
license. The inspectors reviewed selected procedures and records, observed activities, and
interviewed personnel.
Dear Mr. Pollock:  
This report documents seven findings of very low safety significance (Green). Six of these
findings were also determined to be violations of NRC requirements. However, because of their
On March 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection  
very low safety significance, and because the findings were entered into your corrective action
at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report  
program, the NRC is treating these findings as non-cited violations (NCVs) consistent with
documents the inspection results, which were discussed on April 15, 2009, with you and other  
Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you
members of your staff.  
should provide a written response within 30 days of the date of this inspection report, with the
basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk,
The inspection examined activities conducted under your license as they relate to safety and  
Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director,
compliance with the Commissions rules and regulations, and with the conditions of your  
Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC
license. The inspectors reviewed selected procedures and records, observed activities, and  
20555-0001; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 2.
interviewed personnel.  
In addition, if you disagree with the characterization of any finding, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
This report documents seven findings of very low safety significance (Green). Six of these  
disagreement, to the Regional Administrator and the NRC Resident Inspectors at Indian Point
findings were also determined to be violations of NRC requirements. However, because of their  
Nuclear Generating Unit 2. The information you provide will be considered in accordance with
very low safety significance, and because the findings were entered into your corrective action  
Inspection Manual Chapter 0305.
program, the NRC is treating these findings as non-cited violations (NCVs) consistent with  
Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you  
should provide a written response within 30 days of the date of this inspection report, with the  
basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk,  
Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director,  
Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC  
20555-0001; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 2.
In addition, if you disagree with the characterization of any finding, you should provide a  
response within 30 days of the date of this inspection report, with the basis for your  
disagreement, to the Regional Administrator and the NRC Resident Inspectors at Indian Point  
Nuclear Generating Unit 2. The information you provide will be considered in accordance with  
Inspection Manual Chapter 0305.  
ENT000427
Submitted:  March 30, 2012


J. Pollock                                     2
J. Pollock  
In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules
2  
of Practice, a copy of this letter, its enclosure, and your response (if any) will be available
electronically for public inspection in the NRC Public Document Room of from the Publicly
In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules  
Available Records (PARS) component of the NRCs document system (ADAMS).
of Practice, a copy of this letter, its enclosure, and your response (if any) will be available  
ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html
electronically for public inspection in the NRC Public Document Room of from the Publicly  
(the Public Electronic Reading Room).
Available Records (PARS) component of the NRCs document system (ADAMS).  
                                                        Sincerely,
ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html
                                                        /RA/
(the Public Electronic Reading Room).  
                                                        Mel Gray, Chief
                                                        Projects Branch 2
                                                        Division of Reactor Projects
Docket No. 50-247
License No. DPR-26
Enclosure:     Inspection Report No. 05000247/2009002
                w/ Attachment: Supplemental Information
cc w/encl:
Senior Vice President, Entergy Nuclear Operations
Sincerely,  
Vice President, Operations, Entergy Nuclear Operations
Vice President, Oversight, Entergy Nuclear Operations
Senior Manager, Nuclear Safety and Licensing, Entergy Nuclear Operations
Senior Vice President and COO, Entergy Nuclear Operations
Assistant General Counsel, Entergy Nuclear Operations
Manager, Licensing, Entergy Nuclear Operations
C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law
A. Donahue, Mayor, Village of Buchanan
J. G. Testa, Mayor, City of Peekskill
/RA/  
R. Albanese, Four County Coordinator
S. Lousteau, Treasury Department, Entergy Services, Inc.
Chairman, Standing Committee on Energy, NYS Assembly
Chairman, Standing Committee on Environmental Conservation, NYS Assembly
Chairman, Committee on Corporations, Authorities, and Commissions
M. Slobodien, Director, Emergency Planning
P. Eddy, NYS Department of Public Service
Assemblywoman Sandra Galef, NYS Assembly
T. Seckerson, County Clerk, Westchester County Board of Legislators
Mel Gray, Chief  
A. Spano, Westchester County Executive
R. Bondi, Putnam County Executive
C. Vanderhoef, Rockland County Executive
E. A. Diana, Orange County Executive
T. Judson, Central NY Citizens Awareness Network
M. Elie, Citizens Awareness Network
Public Citizen's Critical Mass Energy Project
M. Mariotte, Nuclear Information & Resources Service
Projects Branch 2  
F. Zalcman, Pace Law School, Energy Project
L. Puglisi, Supervisor, Town of Cortlandt
Division of Reactor Projects  
Docket No. 50-247  
License No. DPR-26  
Enclosure:  
Inspection Report No. 05000247/2009002  
w/ Attachment: Supplemental Information  
cc w/encl:  
Senior Vice President, Entergy Nuclear Operations  
Vice President, Operations, Entergy Nuclear Operations  
Vice President, Oversight, Entergy Nuclear Operations  
Senior Manager, Nuclear Safety and Licensing, Entergy Nuclear Operations  
Senior Vice President and COO, Entergy Nuclear Operations  
Assistant General Counsel, Entergy Nuclear Operations  
Manager, Licensing, Entergy Nuclear Operations  
C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law  
A. Donahue, Mayor, Village of Buchanan  
J. G. Testa, Mayor, City of Peekskill  
R. Albanese, Four County Coordinator  
S. Lousteau, Treasury Department, Entergy Services, Inc.  
Chairman, Standing Committee on Energy, NYS Assembly  
Chairman, Standing Committee on Environmental Conservation, NYS Assembly  
Chairman, Committee on Corporations, Authorities, and Commissions  
M. Slobodien, Director, Emergency Planning  
P. Eddy, NYS Department of Public Service  
Assemblywoman Sandra Galef, NYS Assembly  
T. Seckerson, County Clerk, Westchester County Board of Legislators  
A. Spano, Westchester County Executive  
R. Bondi, Putnam County Executive  
C. Vanderhoef, Rockland County Executive  
E. A. Diana, Orange County Executive  
T. Judson, Central NY Citizens Awareness Network  
M. Elie, Citizens Awareness Network  
Public Citizen's Critical Mass Energy Project  
M. Mariotte, Nuclear Information & Resources Service  
F. Zalcman, Pace Law School, Energy Project  
L. Puglisi, Supervisor, Town of Cortlandt  


J. Pollock                                 3
J. Pollock  
Congressman John Hall
3  
Congresswoman Nita Lowey
Senator Kirsten E. Gillibrand
Congressman John Hall  
Senator Charles Schumer
Congresswoman Nita Lowey  
G. Shapiro, Senator Gillibrand 's Staff
Senator Kirsten E. Gillibrand  
J. Riccio, Greenpeace
Senator Charles Schumer  
P. Musegaas, Riverkeeper, Inc.
G. Shapiro, Senator Gillibrand 's Staff  
M. Kaplowitz, Chairman of County Environment & Health Committee
J. Riccio, Greenpeace  
A. Reynolds, Environmental Advocates
P. Musegaas, Riverkeeper, Inc.  
D. Katz, Executive Director, Citizens Awareness Network
M. Kaplowitz, Chairman of County Environment & Health Committee  
K. Coplan, Pace Environmental Litigation Clinic
A. Reynolds, Environmental Advocates  
M. Jacobs, IPSEC
D. Katz, Executive Director, Citizens Awareness Network  
W. Little, Associate Attorney, NYSDEC
K. Coplan, Pace Environmental Litigation Clinic  
M. J. Greene, Clearwater, Inc.
M. Jacobs, IPSEC  
R. Christman, Manager Training and Development
W. Little, Associate Attorney, NYSDEC  
J. Spath, New York State Energy Research, SLO Designee
M. J. Greene, Clearwater, Inc.  
F. Murray, President & CEO, New York State Energy Research
R. Christman, Manager Training and Development
A. J. Kremer, New York Affordable Reliable Electricity Alliance (NY AREA)
J. Spath, New York State Energy Research, SLO Designee  
F. Murray, President & CEO, New York State Energy Research  
A. J. Kremer, New York Affordable Reliable Electricity Alliance (NY AREA)  


J. Pollock                                                         4
J. Pollock  
In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules
4  
of Practice, a copy of this letter, its enclosure, and your response (if any) will be available
electronically for public inspection in the NRC Public Document Room of from the Publicly
In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules  
Available Records (PARS) component of the NRCs document system (ADAMS).
of Practice, a copy of this letter, its enclosure, and your response (if any) will be available  
ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html
electronically for public inspection in the NRC Public Document Room of from the Publicly  
(the Public Electronic Reading Room).
Available Records (PARS) component of the NRCs document system (ADAMS).  
                                                                                  Sincerely,
ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html
                                                                                  /RA/
(the Public Electronic Reading Room).  
                                                                                  Mel Gray, Chief
                                                                                  Projects Branch 2
                                                                                  Division of Reactor Projects
Distribution w/encl: (via E-mail)                                                 C. Hott, DRP, RI, IP2
S. Collins, RA                                                                    D. Hochmuth, DRP, OA
M. Dapas, DRA                                                                    S. Campbell, RI OEDO
D. Lew, DRP                                                                      R. Nelson, NRR
J. Clifford, DRP                                                                  M. Kowal, NRR
M. Gray, DRP                                                                      J. Boska, PM, NRR
Sincerely,  
B. Bickett, DRP                                                                  J. Hughey, NRR
A. Rosebrook, DRP                                                                D. Bearde, DRP
S. McCarver, DRP                                                                  ROPreports@nrc.gov
J. Heinly, DRP                                                                    Region I Docket Room (w/concurrences)
G. Malone, DRP, SRI, IP2
SUNSI Review Complete: ____BSB____ (Reviewers Initial)
DOCUMENT NAME: G:\DRP\BRANCH2\A - INDIAN POINT 2\INSPECTION REPORTS\IP2 IR2009-002\IP2
2009002 REVFINAL.DOC
After declaring this document An Official Agency Record it will be released to the Public
To Receive a copy of this document, indicate in the box: C = Copy without attachment/enclosure E = Copy with attachment/enclosure N = No copy
  Office                 RI/DRP                             RI/DRP                                   RI/DRP
  Name                   GMalone/BSB for                     BBickett/                               MGray/
  Date                   05/14/09                             05/14/09                               05/14/09
                                                    OFFICAL AGENCY RECORD
/RA/  
Mel Gray, Chief  
Projects Branch 2  
Division of Reactor Projects  
Distribution w/encl: (via E-mail)
S. Collins, RA
M. Dapas, DRA
D. Lew, DRP
J. Clifford, DRP 
M. Gray, DRP
B. Bickett, DRP
A. Rosebrook, DRP
S. McCarver, DRP
J. Heinly, DRP 
G. Malone, DRP, SRI, IP2 
C. Hott, DRP, RI, IP2  
D. Hochmuth, DRP, OA  
S. Campbell, RI OEDO
R. Nelson, NRR  
M. Kowal, NRR  
J. Boska, PM, NRR  
J. Hughey, NRR  
D. Bearde, DRP  
ROPreports@nrc.gov  
Region I Docket Room (w/concurrences)  
SUNSI Review Complete: ____BSB____ (Reviewers Initial)  
DOCUMENT NAME: G:\\DRP\\BRANCH2\\A - INDIAN POINT 2\\INSPECTION REPORTS\\IP2 IR2009-002\\IP2  
2009002 REVFINAL.DOC  
After declaring this document An Official Agency Record it will be released to the Public  
To Receive a copy of this document, indicate in the box: C = Copy without attachment/enclosure E = Copy with attachment/enclosure N = No copy  
Office  
RI/DRP  
RI/DRP  
RI/DRP  
Name  
GMalone/BSB for  
BBickett/  
MGray/  
Date  
05/14/09  
05/14/09  
05/14/09  
OFFICAL AGENCY RECORD  


                                      1
1  
                U.S. NUCLEAR REGULATORY COMMISSION
Enclosure 
                                  REGION I
Docket No.:  50-247
U.S. NUCLEAR REGULATORY COMMISSION  
License No.: DPR-26
Report No.:  05000247/2009002
REGION I  
Licensee:   Entergy Nuclear Northeast (Entergy)
Facility:   Indian Point Nuclear Generating Unit 2
Location:   450 Broadway, GSB
            Buchanan, NY 10511-0249
Docket No.:  
Dates:       January 1, 2009 through March 31, 2009
   
Inspectors:  G. Malone, Senior Resident Inspector, Indian Point 2
50-247  
            C. Hott, Resident Inspector, Indian Point 2
            J. Commisky, Health Physics Inspector, Region I
Approved By: Mel Gray, Chief
License No.:
            Projects Branch 2
DPR-26  
            Division of Reactor Projects
                                                                  Enclosure
Report No.:  
   
05000247/2009002  
Licensee:  
Entergy Nuclear Northeast (Entergy)  
Facility:  
Indian Point Nuclear Generating Unit 2  
Location:  
450 Broadway, GSB  
Buchanan, NY 10511-0249  
Dates:
January 1, 2009 through March 31, 2009  
Inspectors:  
   
G. Malone, Senior Resident Inspector, Indian Point 2  
C. Hott, Resident Inspector, Indian Point 2  
J. Commisky, Health Physics Inspector, Region I  
Approved By:
Mel Gray, Chief  
Projects Branch 2  
Division of Reactor Projects  


                                                            2
2  
                                          TABLE OF CONTENTS
Enclosure 
SUMMARY OF FINDINGS ............................................................................................................... 3
TABLE OF CONTENTS  
REPORT DETAILS........................................................................................................................... 8
1. REACTOR SAFETY .................................................................................................................... 8
1R01   Adverse Weather Protection ............................................................................................... 8
1R04   Equipment Alignment ....................................................................................................... 10
SUMMARY OF FINDINGS ............................................................................................................... 3  
1R05   Fire Protection .................................................................................................................. 10
1R07   Heat Sink Performance .................................................................................................... 14
REPORT DETAILS ........................................................................................................................... 8  
1R11   Licensed Operator Requalification Program ..................................................................... 15
1R12   Maintenance Effectiveness ............................................................................................... 15
1. REACTOR SAFETY .................................................................................................................... 8  
1R13   Maintenance Risk Assessments and Emergent Work Control .......................................... 18
1R01  
1R15   Operability Evaluations ..................................................................................................... 19
Adverse Weather Protection ............................................................................................... 8  
1R18   Plant Modifications ........................................................................................................... 20
1R04  
1R19   Post-Maintenance Testing ................................................................................................ 21
Equipment Alignment ....................................................................................................... 10  
1R22   Surveillance Testing ......................................................................................................... 21
1R05  
1EP6   Drill Evaluation ................................................................................................................ 24
Fire Protection .................................................................................................................. 10  
2. RADIATION SAFETY ................................................................................................................ 24
1R07  
2OS1 Access Control to Radiologically Significant Areas ........................................................... 24
Heat Sink Performance .................................................................................................... 14  
2OS2 ALARA Planning and Controls.......................................................................................... 28
1R11  
4. OTHER ACTIVITIES.................................................................................................................. 30
Licensed Operator Requalification Program ..................................................................... 15  
4OA1 Performance Indicator Verification ................................................................................... 30
1R12  
4OA2 Identification and Resolution of Problems ......................................................................... 31
Maintenance Effectiveness ............................................................................................... 15  
4OA3 Event Followup ................................................................................................................. 31
1R13  
4OA5 Other Activities ................................................................................................................. 32
Maintenance Risk Assessments and Emergent Work Control .......................................... 18  
4OA6 Meetings........................................................................................................................... 33
1R15  
ATTACHMENT: SUPPLEMENTAL INFORMATION .................................................................... A-1
Operability Evaluations ..................................................................................................... 19  
SUPPLEMENTAL INFORMATION ............................................................................................... A-1
1R18  
KEY POINTS OF CONTACT ........................................................................................................ A-1
Plant Modifications ........................................................................................................... 20  
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ............................................................. A-1
1R19  
LIST OF DOCUMENTS REVIEWED ............................................................................................ A-2
Post-Maintenance Testing ................................................................................................ 21  
LIST OF ACRONYMS .................................................................................................................. A-8
1R22  
                                                                                                                        Enclosure
Surveillance Testing ......................................................................................................... 21  
1EP6  
Drill Evaluation ................................................................................................................ 24  
2. RADIATION SAFETY ................................................................................................................ 24  
2OS1  
Access Control to Radiologically Significant Areas ........................................................... 24  
2OS2  
ALARA Planning and Controls .......................................................................................... 28  
4. OTHER ACTIVITIES .................................................................................................................. 30  
4OA1  
Performance Indicator Verification ................................................................................... 30  
4OA2  
Identification and Resolution of Problems ......................................................................... 31  
4OA3  
Event Followup ................................................................................................................. 31  
4OA5  
Other Activities ................................................................................................................. 32  
4OA6  
Meetings ........................................................................................................................... 33  
ATTACHMENT: SUPPLEMENTAL INFORMATION .................................................................... A-1  
SUPPLEMENTAL INFORMATION ............................................................................................... A-1  
KEY POINTS OF CONTACT ........................................................................................................ A-1  
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ............................................................. A-1  
LIST OF DOCUMENTS REVIEWED ............................................................................................ A-2  
LIST OF ACRONYMS .................................................................................................................. A-8  


                                                    3
3  
                                        SUMMARY OF FINDINGS
Enclosure 
IR 05000247/2009-002; 01/01/2009 - 03/31/2009; Indian Point Nuclear Generating (Indian
SUMMARY OF FINDINGS  
Point) Unit 2; Adverse Weather Protection; Fire Protection; Maintenance Effectiveness;
Maintenance Risk Assessments; Surveillance Testing; and Radiological Access Control.
This report covered a three-month period of inspection by resident and region based inspectors.
IR 05000247/2009-002; 01/01/2009 - 03/31/2009; Indian Point Nuclear Generating (Indian  
Seven findings of very low significance (Green) were identified, six of which were also
Point) Unit 2; Adverse Weather Protection; Fire Protection; Maintenance Effectiveness;  
determined to be non-cited violations (NCV). The significance of most findings is indicated by
Maintenance Risk Assessments; Surveillance Testing; and Radiological Access Control.  
their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
Significance Determination Process. The cross-cutting aspect for each finding was
This report covered a three-month period of inspection by resident and region based inspectors.
determined using IMC 0305, Operating Reactor Assessment Program. Findings for which the
Seven findings of very low significance (Green) were identified, six of which were also  
significance determination process (SDP) does not apply may be Green, or be assigned a
determined to be non-cited violations (NCV). The significance of most findings is indicated by  
severity level after NRC management review. The NRCs program for overseeing safe
their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,  
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Significance Determination Process. The cross-cutting aspect for each finding was  
Oversight Process, Revision 4, dated December 2006.
determined using IMC 0305, Operating Reactor Assessment Program. Findings for which the  
A.     NRC-Identified and Self-Revealing Findings
significance determination process (SDP) does not apply may be Green, or be assigned a  
        Cornerstone: Initiating Events
severity level after NRC management review. The NRCs program for overseeing safe  
    *   Green. The inspectors identified a NCV of very low safety significance related to 10 CFR
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor  
        50, Appendix B, Criterion XVI, Corrective Actions, because Entergy did not promptly
Oversight Process, Revision 4, dated December 2006.  
        identify and correct an adverse condition related to an electrical fault. Specifically,
        personnel did not identify a safety-related cubicle had experienced an electrical fault
A.  
        prior to replacement of upstream fuses and restoration of power to the damaged cubicle.
NRC-Identified and Self-Revealing Findings  
        Entergy entered the issue into the corrective action program as IP2-2009-00342 and
        IP2-2009-00483, trained all operations personnel on the requirements to replace fuses
Cornerstone: Initiating Events  
        and re-energize electrical equipment, and plans to revise the operations procedure for
        operating electrical equipment.
*  
        This issue was more than minor because the finding was associated with the external
Green. The inspectors identified a NCV of very low safety significance related to 10 CFR  
        factors attribute of the Initiating Events cornerstone and impacted the cornerstone
50, Appendix B, Criterion XVI, Corrective Actions, because Entergy did not promptly  
        objective of limiting the likelihood of those events that upset plant stability and challenge
identify and correct an adverse condition related to an electrical fault. Specifically,  
        critical safety systems during shutdown as well as power operations. The inspectors
personnel did not identify a safety-related cubicle had experienced an electrical fault  
        determined that the issue increased the likelihood of a fire in the emergency diesel
prior to replacement of upstream fuses and restoration of power to the damaged cubicle.
        generator (EDG) building. The condition was evaluated by a Senior Reactor Analyst
Entergy entered the issue into the corrective action program as IP2-2009-00342 and  
        utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection Significance Determination
IP2-2009-00483, trained all operations personnel on the requirements to replace fuses  
        Process. It was determined that in the event of a fire consuming the MCC, no transient
and re-energize electrical equipment, and plans to revise the operations procedure for  
        would be placed on the plant and no components required to safely shutdown the plant
operating electrical equipment.  
        would be impacted. As a result, in accordance with task 2.3.5 of Appendix F, the issue
        was screened to Green.
This issue was more than minor because the finding was associated with the external  
        The inspectors determined that a cross-cutting aspect was associated with this finding
factors attribute of the Initiating Events cornerstone and impacted the cornerstone  
        in the area of human performance related to conservative decision making. Specifically,
objective of limiting the likelihood of those events that upset plant stability and challenge  
        Entergys decision-making was non-conservative related to its decisions on the process
critical safety systems during shutdown as well as power operations. The inspectors  
        used to identify the source of the acrid odor; re-energize the damaged electrical
determined that the issue increased the likelihood of a fire in the emergency diesel  
        equipment; and keep a damaged electrical component energized for 14 days prior to its
generator (EDG) building. The condition was evaluated by a Senior Reactor Analyst  
        removal from the MCC. [H.1(b) per IMC 0305] (Section 1R05)
utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection Significance Determination  
                                                                                            Enclosure
Process. It was determined that in the event of a fire consuming the MCC, no transient  
would be placed on the plant and no components required to safely shutdown the plant  
would be impacted. As a result, in accordance with task 2.3.5 of Appendix F, the issue  
was screened to Green.  
The inspectors determined that a cross-cutting aspect was associated with this finding  
in the area of human performance related to conservative decision making. Specifically,  
Entergys decision-making was non-conservative related to its decisions on the process  
used to identify the source of the acrid odor; re-energize the damaged electrical  
equipment; and keep a damaged electrical component energized for 14 days prior to its  
removal from the MCC. [H.1(b) per IMC 0305] (Section 1R05)  


                                              4
4  
* Green. The inspectors identified a NCV of very low safety significance related to TS
Enclosure 
  5.4.1, Administrative Controls: Procedures, because Entergy did not maintain an
*  
  adequate maintenance procedure for a safety-related electrical motor control center
Green. The inspectors identified a NCV of very low safety significance related to TS  
  (MCC). Specifically, the eight-year maintenance procedure for the affected EDG
5.4.1, Administrative Controls: Procedures, because Entergy did not maintain an  
  ventilation MCC did not contain an adequate method to identify high resistance
adequate maintenance procedure for a safety-related electrical motor control center  
  connections within the cubicle as was expected in the applicable preventative
(MCC). Specifically, the eight-year maintenance procedure for the affected EDG  
  maintenance industry template. Subsequently, a high resistance connection within the
ventilation MCC did not contain an adequate method to identify high resistance  
  MCC developed into a phase-to-phase electrical fault on January 28, 2009. Entergy
connections within the cubicle as was expected in the applicable preventative  
  entered the issue into the corrective action program, scoped the affected MCC and 21
maintenance industry template. Subsequently, a high resistance connection within the  
  additional MCCs into the sites thermography program, and planned to revise the
MCC developed into a phase-to-phase electrical fault on January 28, 2009. Entergy  
  maintenance procedure.
entered the issue into the corrective action program, scoped the affected MCC and 21  
  This issue was more than minor because the finding was associated with the external
additional MCCs into the sites thermography program, and planned to revise the  
  factors attribute of the Initiating Events cornerstone and impacted the cornerstone
maintenance procedure.  
  objective of limiting the likelihood of those events that upset plant stability and challenge
  critical safety systems during shutdown as well as power operations. Specifically, the
This issue was more than minor because the finding was associated with the external  
  high resistance connection degraded into a phase-to-phase fault and increased the
factors attribute of the Initiating Events cornerstone and impacted the cornerstone  
  likelihood of a fire in the EDG building. The condition was evaluated by a Senior
objective of limiting the likelihood of those events that upset plant stability and challenge  
  Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection Significance
critical safety systems during shutdown as well as power operations. Specifically, the  
  Determination Process. It was determined that in the event of a fire consuming the
high resistance connection degraded into a phase-to-phase fault and increased the  
  MCC, no transient would be placed on the plant and no components required to safely
likelihood of a fire in the EDG building. The condition was evaluated by a Senior  
  shutdown the plant would be impacted. As a result, in accordance with task 2.3.5 of
Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection Significance  
  Appendix F, the issue was screened to Green.
Determination Process. It was determined that in the event of a fire consuming the  
  The inspectors determined that the finding had a cross-cutting aspect associated with
MCC, no transient would be placed on the plant and no components required to safely  
  the area of problem identification and resolution related to the use of operating
shutdown the plant would be impacted. As a result, in accordance with task 2.3.5 of  
  experience (OE). Specifically, Entergy personnel did not implement industry
Appendix F, the issue was screened to Green.  
  recommended practices, or an alternate equivalent method, for identifying high
  resistance connections in electrical switchgear. [P.2(b) per IMC 0305] (Section 1R12)
The inspectors determined that the finding had a cross-cutting aspect associated with  
  Cornerstone: Mitigating Systems
the area of problem identification and resolution related to the use of operating  
* Green. The inspectors identified a finding of very low safety significance because
experience (OE). Specifically, Entergy personnel did not implement industry  
  Entergy personnel did not adequately implement procedure EN-LI-102, Corrective Action
recommended practices, or an alternate equivalent method, for identifying high  
  Process, and promptly identify a condition adverse to quality associated with open
resistance connections in electrical switchgear. [P.2(b) per IMC 0305] (Section 1R12)  
  louvers in a fire protection pump room following pump testing on January 14, 2009. The
  open louvers resulted in freezing conditions in fire protection piping located in the room
Cornerstone: Mitigating Systems  
  and cracked two six-inch header isolation valves on January 17, 2009. Entergy entered
  the issue into the corrective action program and performed a site-wide extent-of-
*  
  condition walkdown of louvers.
Green. The inspectors identified a finding of very low safety significance because  
  The finding was more than minor because it was associated with the protection against
Entergy personnel did not adequately implement procedure EN-LI-102, Corrective Action  
  external factors attribute of the Mitigating Systems cornerstone and it affected the
Process, and promptly identify a condition adverse to quality associated with open  
  cornerstone objective of ensuring the reliability of systems that respond to initiating
louvers in a fire protection pump room following pump testing on January 14, 2009. The  
  events to prevent undesirable consequences. This finding was evaluated using Phase
open louvers resulted in freezing conditions in fire protection piping located in the room  
  1 of IMC 0609 Appendix F, Fire Protection Significance Determination Process. The
and cracked two six-inch header isolation valves on January 17, 2009. Entergy entered  
  inspectors determined the issue was of very low safety significance (Green) because
the issue into the corrective action program and performed a site-wide extent-of-
  the cracked valves were easily isolated and did not pass sufficient water to render the
condition walkdown of louvers.  
  fire header non-functional (low degradation rating).
                                                                                      Enclosure
The finding was more than minor because it was associated with the protection against  
external factors attribute of the Mitigating Systems cornerstone and it affected the  
cornerstone objective of ensuring the reliability of systems that respond to initiating  
events to prevent undesirable consequences. This finding was evaluated using Phase  
1 of IMC 0609 Appendix F, Fire Protection Significance Determination Process. The  
inspectors determined the issue was of very low safety significance (Green) because  
the cracked valves were easily isolated and did not pass sufficient water to render the  
fire header non-functional (low degradation rating).  


                                              5
5  
  The inspectors determined that the finding had a cross-cutting aspect in the area of
Enclosure 
  human performance related to work practices - human error prevention techniques.
The inspectors determined that the finding had a cross-cutting aspect in the area of  
  Specifically, Entergy personnel that routinely tour the 11 fire pump house did not
human performance related to work practices - human error prevention techniques.
  question the abnormally cold room temperatures. [H.4(a) per IMC 0305] (Section 1R01)
Specifically, Entergy personnel that routinely tour the 11 fire pump house did not  
* Green. The inspectors identified a NCV of very low safety significance related to License
question the abnormally cold room temperatures. [H.4(a) per IMC 0305] (Section 1R01)  
  Condition 2.K., fire protection program, because personnel did not promptly identify and
  correct a degraded three-hour rated fire door latch mechanism on the west entrance of
*  
  the 480-Volt switchgear room. Specifically, inspectors identified the fire door in a non-
Green. The inspectors identified a NCV of very low safety significance related to License  
  functional state on several instances over the course of a month. Entergy personnel
Condition 2.K., fire protection program, because personnel did not promptly identify and  
  replaced the fire door latch mechanism on March 3, 2009. This issue was entered into
correct a degraded three-hour rated fire door latch mechanism on the west entrance of  
  the corrective action program as six condition reports spanning several weeks and
the 480-Volt switchgear room. Specifically, inspectors identified the fire door in a non-
  included an extent of condition walkdown of site fire doors.
functional state on several instances over the course of a month. Entergy personnel  
  The finding was more than minor because it is associated with the protection against
replaced the fire door latch mechanism on March 3, 2009. This issue was entered into  
  external factors attribute of the Mitigating Systems cornerstone and affected the
the corrective action program as six condition reports spanning several weeks and  
  cornerstone objective of ensuring the reliability of systems that respond to initiating
included an extent of condition walkdown of site fire doors.
  events to prevent undesirable consequences. This fire door, when degraded, impacts
  the reliability of mitigating systems in the 480-Volt switchgear room that are relied upon
The finding was more than minor because it is associated with the protection against  
  during a postulated large fire in the turbine building, and vice versa. This finding was
external factors attribute of the Mitigating Systems cornerstone and affected the  
  evaluated using Phase 1 of IMC 0609 Appendix F, Fire Protection Significance
cornerstone objective of ensuring the reliability of systems that respond to initiating  
  Determination Process. Since the area in question had a fire watch posted during the
events to prevent undesirable consequences. This fire door, when degraded, impacts  
  time the door was degraded for an unrelated issue, an adequate level of protection was
the reliability of mitigating systems in the 480-Volt switchgear room that are relied upon  
  maintained to compensate for the degraded door. As such, according to task 1.3.1, the
during a postulated large fire in the turbine building, and vice versa. This finding was  
  inspectors determined the finding was Green.
evaluated using Phase 1 of IMC 0609 Appendix F, Fire Protection Significance  
  The inspectors determined that the finding had a cross-cutting aspect in the area of
Determination Process. Since the area in question had a fire watch posted during the  
  problem identification and resolution because Entergy personnel did not thoroughly
time the door was degraded for an unrelated issue, an adequate level of protection was  
  evaluate a degraded fire door latch on several occasions, such that the resolution of the
maintained to compensate for the degraded door. As such, according to task 1.3.1, the  
  problems addressed the causes. [P.1(c) per IMC 0305] (Section 1R05)
inspectors determined the finding was Green.
* Green. The inspectors identified a NCV of very low safety significance related to 10 CFR
  50.65(a)(4), because Entergy personnel did not adequately assess the risk associated
The inspectors determined that the finding had a cross-cutting aspect in the area of  
  with the unavailability of the Refueling Water Storage Tank (RWST) level indication
problem identification and resolution because Entergy personnel did not thoroughly  
  during planned maintenance on the level transmitters and instrumentation. Entergy
evaluate a degraded fire door latch on several occasions, such that the resolution of the  
  entered the issue into the corrective action program (CR-IP2-2009-00342), updated the
problems addressed the causes. [P.1(c) per IMC 0305] (Section 1R05)  
  risk model to include the maintenance activity, assessed the risk, and appropriately
  coded the maintenance activity to ensure it would be risk assessed in the future.
*  
  The inspectors determined that this finding was more than minor because it was a
Green. The inspectors identified a NCV of very low safety significance related to 10 CFR  
  maintenance risk assessment issue in which personnel did not consider risk significant
50.65(a)(4), because Entergy personnel did not adequately assess the risk associated  
  SSCs that were unavailable during maintenance. The RWST level indication is
with the unavailability of the Refueling Water Storage Tank (RWST) level indication  
  specifically listed in Table 2 of the plant specific Phase 2 SDP risk-informed inspection
during planned maintenance on the level transmitters and instrumentation. Entergy  
  notebook. The inspectors determined the significance of this issue in accordance with
entered the issue into the corrective action program (CR-IP2-2009-00342), updated the  
  IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management
risk model to include the maintenance activity, assessed the risk, and appropriately  
  Significance Determination Process. The inspectors determined that this finding was of
coded the maintenance activity to ensure it would be risk assessed in the future.  
  very low safety significance because the Incremental Core Damage Probability Deficit
  was less than 1E-6.
The inspectors determined that this finding was more than minor because it was a  
  The inspectors determined that the finding had a cross-cutting aspect in the area of
maintenance risk assessment issue in which personnel did not consider risk significant  
  human performance related to work control. Specifically, Entergy personnel did not
SSCs that were unavailable during maintenance. The RWST level indication is  
                                                                                      Enclosure
specifically listed in Table 2 of the plant specific Phase 2 SDP risk-informed inspection  
notebook. The inspectors determined the significance of this issue in accordance with  
IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management  
Significance Determination Process. The inspectors determined that this finding was of  
very low safety significance because the Incremental Core Damage Probability Deficit  
was less than 1E-6.  
The inspectors determined that the finding had a cross-cutting aspect in the area of  
human performance related to work control. Specifically, Entergy personnel did not  


                                              6
6  
  appropriately plan work activities by incorporating risk insights for affected plant
Enclosure 
  equipment. [H.3(a) per IMC 0305] (Section 1R13)
appropriately plan work activities by incorporating risk insights for affected plant  
* Green. The inspectors identified a NCV of very low safety significance related to 10
equipment. [H.3(a) per IMC 0305] (Section 1R13)  
  CFR 50.55a, Codes and standards, because Entergys procedure, 2-PT-Q031A for an
  auxiliary component cooling water pump, did not contain appropriate acceptance criteria
*  
  for positively determining that safety-related check valves performed their safety function
Green. The inspectors identified a NCV of very low safety significance related to 10  
  when required in accordance with the American Society of Mechanical Engineers
CFR 50.55a, Codes and standards, because Entergys procedure, 2-PT-Q031A for an  
  (ASME) OM Code. Specifically, the test used reverse rotation of a parallel pump to
auxiliary component cooling water pump, did not contain appropriate acceptance criteria  
  verify that the pumps discharge check valve was closed although previous site-specific
for positively determining that safety-related check valves performed their safety function  
  experience demonstrated that the pump impeller would not rotate backwards when the
when required in accordance with the American Society of Mechanical Engineers  
  check valve was stuck open. Entergy entered this issue into their corrective action
(ASME) OM Code. Specifically, the test used reverse rotation of a parallel pump to  
  program as CR-2009-1312.
verify that the pumps discharge check valve was closed although previous site-specific  
  The inspectors determined that the performance deficiency was greater than minor
experience demonstrated that the pump impeller would not rotate backwards when the  
  because it was associated with the procedure quality attribute of the Mitigating System
check valve was stuck open. Entergy entered this issue into their corrective action  
  cornerstone and it adversely affected the cornerstones objective to ensure the reliability
program as CR-2009-1312.  
  of systems that respond to initiating events to prevent undesirable consequences.
  Specifically, the test criterion used in procedure 2-PT-Q013A did not ensure that valve
The inspectors determined that the performance deficiency was greater than minor  
  755A reliably performed its safety function when tested as demonstrated by testing
because it was associated with the procedure quality attribute of the Mitigating System  
  performed in January 2005. The inspectors determined that the performance deficiency
cornerstone and it adversely affected the cornerstones objective to ensure the reliability  
  was of very low safety significance (Green) IMC 0609, Attachment 4, Phase 1 - Initial
of systems that respond to initiating events to prevent undesirable consequences.
  Screening and Characterization of Findings. Specifically, the inspectors determined
Specifically, the test criterion used in procedure 2-PT-Q013A did not ensure that valve  
  that this finding was of very low safety significance because the finding did not result in
755A reliably performed its safety function when tested as demonstrated by testing  
  a loss of safety function and did not screen as potentially risk-significant due to external
performed in January 2005. The inspectors determined that the performance deficiency  
  events initiating events.
was of very low safety significance (Green) IMC 0609, Attachment 4, Phase 1 - Initial  
  The inspectors determined the finding had a cross-cutting aspect related to effective
Screening and Characterization of Findings. Specifically, the inspectors determined  
  corrective actions in the corrective action program component of the problem
that this finding was of very low safety significance because the finding did not result in  
  identification and resolution area. Specifically, Entergy personnel did not implement
a loss of safety function and did not screen as potentially risk-significant due to external  
  effective corrective actions to resolve the testing inadequacy since 2005 and during
events initiating events.  
  subsequent quarterly testing. [P.1(d) per IMC 0305] (Section 1R22)
  Cornerstone: Occupational Radiation Safety
The inspectors determined the finding had a cross-cutting aspect related to effective  
* Green. The inspectors identified a NCV of very low safety significance related to
corrective actions in the corrective action program component of the problem  
  Technical Specification 5.4.1.a, Procedures, because Entergy personnel did not
identification and resolution area. Specifically, Entergy personnel did not implement  
  generate condition reports or investigation paperwork for multiple high dose-rate alarms
effective corrective actions to resolve the testing inadequacy since 2005 and during  
  as required by station procedures. Specifically, personnel did not generate the required
subsequent quarterly testing. [P.1(d) per IMC 0305] (Section 1R22)  
  condition reports and adequately document the investigations for six instances of
  unplanned or un-briefed electronic dosimeter alarms that occurred between January
Cornerstone: Occupational Radiation Safety  
  2009 and March 2009. The performance deficiency resulted in workers receiving
  unanticipated dose rate alarms with no formally-documented investigation prior to
*  
  returning to work in a Radiologically Controlled Area. Entergy entered the finding into
Green. The inspectors identified a NCV of very low safety significance related to  
  the corrective action program as condition report CR-IP3-2009-01253 and 01318.
Technical Specification 5.4.1.a, Procedures, because Entergy personnel did not  
  The finding is more than minor because it is associated with the Occupational Radiation
generate condition reports or investigation paperwork for multiple high dose-rate alarms  
  Safety cornerstone attribute of programs and process, and adversely affected the
as required by station procedures. Specifically, personnel did not generate the required  
  objective to ensure adequate protection of worker health and safety from exposure to
condition reports and adequately document the investigations for six instances of  
  radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and
unplanned or un-briefed electronic dosimeter alarms that occurred between January  
  implement programs to keep exposures as low as reasonably achievable, because
2009 and March 2009. The performance deficiency resulted in workers receiving  
                                                                                      Enclosure
unanticipated dose rate alarms with no formally-documented investigation prior to  
returning to work in a Radiologically Controlled Area. Entergy entered the finding into  
the corrective action program as condition report CR-IP3-2009-01253 and 01318.  
The finding is more than minor because it is associated with the Occupational Radiation  
Safety cornerstone attribute of programs and process, and adversely affected the  
objective to ensure adequate protection of worker health and safety from exposure to  
radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and  
implement programs to keep exposures as low as reasonably achievable, because  


                                            7
7  
  multiple examples were identified regarding the failure to satisfy station radiation
Enclosure 
  protection procedures. Using the Occupational Radiation Safety Significance
multiple examples were identified regarding the failure to satisfy station radiation  
  Determination Process, the inspectors determined that the finding was of very low safety
protection procedures. Using the Occupational Radiation Safety Significance  
  significance (Green) because it did not involve: (1) as low as is reasonably achievable
Determination Process, the inspectors determined that the finding was of very low safety  
  planning and controls, (2) an overexposure of an individual, (3) a substantial potential for
significance (Green) because it did not involve: (1) as low as is reasonably achievable  
  overexposure, or (4) an impaired ability to assess dose.
planning and controls, (2) an overexposure of an individual, (3) a substantial potential for  
  The inspectors determined that the finding had a cross-cutting aspect related to
overexposure, or (4) an impaired ability to assess dose.  
  procedural adherence in the work practices component of the human performance area.
  Specifically, Entergy personnel did not follow procedures to generate condition reports
The inspectors determined that the finding had a cross-cutting aspect related to  
  and document investigations when high dose-rate alarms were received by workers.
procedural adherence in the work practices component of the human performance area.
  [H.4(b) per IMC 0305] (Section 2OS1)
Specifically, Entergy personnel did not follow procedures to generate condition reports  
B. Licensee-Identified Violations
and document investigations when high dose-rate alarms were received by workers.
  None.
[H.4(b) per IMC 0305] (Section 2OS1)  
                                                                                      Enclosure
B.  
Licensee-Identified Violations
None.  


                                                  8
8  
                                        REPORT DETAILS
Enclosure 
Summary of Plant Status
REPORT DETAILS  
Indian Point Nuclear Generating (Indian Point) Unit 2 began the inspection period at full reactor
power and remained at or near full power during the quarter.
1.     REACTOR SAFETY
Summary of Plant Status  
      Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01 - 1 sample)
Indian Point Nuclear Generating (Indian Point) Unit 2 began the inspection period at full reactor  
      Impending Adverse Weather
power and remained at or near full power during the quarter.  
   a.   Inspection Scope
        The inspectors reviewed the overall preparations and protection of risk-significant
1.  
        systems for extremely cold weather conditions from January 14 - 19, 2009. The
REACTOR SAFETY  
        inspectors reviewed and assessed implementation of the sites adverse weather
        preparation procedures and compensatory measures for the affected conditions before
        the onset of and during the cold weather conditions. This included verification that
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
        operator actions defined in their adverse weather procedure maintain readiness of
        essential systems that are vulnerable to freezing temperatures. The inspectors verified
1R01 Adverse Weather Protection (71111.01 - 1 sample)  
        Entergy personnel implemented periodic equipment walkdowns or other measures to
        ensure the condition of plant equipment was operable.
        The inspectors also reviewed Entergys corrective action program to review previous
Impending Adverse Weather  
        issues associated with cold weather preparations and freezing conditions. Documents
        reviewed are listed in the attachment.
   a.  
  b.     Findings
Inspection Scope  
        Introduction. The inspectors identified a Green finding because Entergy personnel did
        not adequately implement procedure EN-LI-102, Corrective Action Process, and
        promptly identify a condition adverse to quality associated with stuck-open louvers in a
The inspectors reviewed the overall preparations and protection of risk-significant  
        fire protection pump room following pump testing on January 14, 2009.
systems for extremely cold weather conditions from January 14 - 19, 2009. The  
        Description. On January 17, 2009, during a period of sustained cold weather which
inspectors reviewed and assessed implementation of the sites adverse weather  
        included sub-zero temperatures, control room personnel received a fire panel trouble
preparation procedures and compensatory measures for the affected conditions before  
        alarm indicative of a low-pressure condition in the fire header and dispatched a plant
the onset of and during the cold weather conditions. This included verification that  
        operator to investigate. The operator identified spraying water from the body of a
operator actions defined in their adverse weather procedure maintain readiness of  
        ruptured six-inch fire protection valve located in the 11 fire pump house. The operator
essential systems that are vulnerable to freezing temperatures. The inspectors verified  
        isolated the broken valve from the fire header by shutting a manually-operated upstream
Entergy personnel implemented periodic equipment walkdowns or other measures to  
        valve which stopped the water spray. In addition, the operator observed that the pump
ensure the condition of plant equipment was operable.  
        house room was significantly colder than expected and subsequently identified the
        rooms ventilation louvers to the outside were mechanically bound in the open position.
The inspectors also reviewed Entergys corrective action program to review previous  
        The operator disconnected the louver linkage and manually shut the louvers.
issues associated with cold weather preparations and freezing conditions. Documents  
                                                                                        Enclosure
reviewed are listed in the attachment.  
   
b.  
Findings  
Introduction. The inspectors identified a Green finding because Entergy personnel did  
not adequately implement procedure EN-LI-102, Corrective Action Process, and  
promptly identify a condition adverse to quality associated with stuck-open louvers in a  
fire protection pump room following pump testing on January 14, 2009.  
Description. On January 17, 2009, during a period of sustained cold weather which  
included sub-zero temperatures, control room personnel received a fire panel trouble  
alarm indicative of a low-pressure condition in the fire header and dispatched a plant  
operator to investigate. The operator identified spraying water from the body of a  
ruptured six-inch fire protection valve located in the 11 fire pump house. The operator  
isolated the broken valve from the fire header by shutting a manually-operated upstream  
valve which stopped the water spray. In addition, the operator observed that the pump  
house room was significantly colder than expected and subsequently identified the  
rooms ventilation louvers to the outside were mechanically bound in the open position.
The operator disconnected the louver linkage and manually shut the louvers.  


                                            9
9  
On January 21, 2009, the inspectors identified a second six inch valve that was cracked
Enclosure 
due to the previous cold weather (freezing) conditions in the fire pump house. Entergy
On January 21, 2009, the inspectors identified a second six inch valve that was cracked  
personnel entered this issue into the corrective action program and performed site
due to the previous cold weather (freezing) conditions in the fire pump house. Entergy  
walkdowns to identify additional adverse conditions associated with the cold weather.
personnel entered this issue into the corrective action program and performed site  
walkdowns to identify additional adverse conditions associated with the cold weather.  
The inspectors determined that Entergy did not fully implement Entergy procedure EN-
The inspectors determined that Entergy did not fully implement Entergy procedure EN-
LI-102, Corrective Action Process. Specifically, EN-LI-102 requires plant personnel to
LI-102, Corrective Action Process. Specifically, EN-LI-102 requires plant personnel to  
identify adverse conditions, including cold-weather related conditions, and then enter
identify adverse conditions, including cold-weather related conditions, and then enter  
them into the CAP for resolution. Attachment 9.2 of the procedure provides examples of
them into the CAP for resolution. Attachment 9.2 of the procedure provides examples of  
adverse conditions expected to be reported; Section 1 of the Attachment contains
adverse conditions expected to be reported; Section 1 of the Attachment contains  
examples of operational conditions requiring entry into the CAP including "events or
examples of operational conditions requiring entry into the CAP including "events or  
conditions that could negatively impact reliability or availability." Additionally, plant
conditions that could negatively impact reliability or availability." Additionally, plant  
operators should have had heightened awareness to cold weather conditions because
operators should have had heightened awareness to cold weather conditions because  
Entergy procedure OAP-008, "Severe Weather Preparations," requires in step 4.3.7,
Entergy procedure OAP-008, "Severe Weather Preparations," requires in step 4.3.7,  
when freezing conditions are expected, that increased monitoring of plant areas to
when freezing conditions are expected, that increased monitoring of plant areas to  
monitor for adverse effects on plant equipment and verify that adequate protection is
monitor for adverse effects on plant equipment and verify that adequate protection is  
provided. Operations personnel did not identify abnormal conditions in the 11 fire pump
provided. Operations personnel did not identify abnormal conditions in the 11 fire pump  
room that led to the freezing and subsequent rupture of fire protection components.
room that led to the freezing and subsequent rupture of fire protection components.  
The inspectors determined it was reasonable for Entergy personnel to identify this issue
because operators should have identified that the louvers failed to shut following a
The inspectors determined it was reasonable for Entergy personnel to identify this issue  
routine operations test of 11 fire pump on January 14, 2009. In addition, operators
because operators should have identified that the louvers failed to shut following a  
perform tours of the pump house every 12 hours and should have identified the room
routine operations test of 11 fire pump on January 14, 2009. In addition, operators  
was much colder than normal.
perform tours of the pump house every 12 hours and should have identified the room  
Analysis. The inspectors identified a performance deficiency because Entergy
was much colder than normal.  
personnel did not implement procedure guidance and identify stuck open louvers and a
subsequent second cracked fire header valve in the 11 fire pump house. The finding
Analysis. The inspectors identified a performance deficiency because Entergy  
was more than minor because it was associated with the protection against external
personnel did not implement procedure guidance and identify stuck open louvers and a  
factors attribute of the Mitigating Systems cornerstone and it affected the cornerstone
subsequent second cracked fire header valve in the 11 fire pump house. The finding  
objective of ensuring the reliability of systems that respond to initiating events to prevent
was more than minor because it was associated with the protection against external  
undesirable consequences. Specifically, the failure of the six-inch valves impacted the
factors attribute of the Mitigating Systems cornerstone and it affected the cornerstone  
reliability of the fire header until the ruptured valve was isolated.
objective of ensuring the reliability of systems that respond to initiating events to prevent  
This finding was evaluated using Phase 1 of Inspection Manual Chapter (IMC) 0609
undesirable consequences. Specifically, the failure of the six-inch valves impacted the  
Appendix F, Fire Protection Significance Determination Process. The inspectors
reliability of the fire header until the ruptured valve was isolated.
determined the issue was of very low safety significance (Green) because the cracked
fire valves were easily isolated and did not pass sufficient water to render the fire
This finding was evaluated using Phase 1 of Inspection Manual Chapter (IMC) 0609  
header non-functional. Specifically, the inspectors assigned a low degradation rating to
Appendix F, Fire Protection Significance Determination Process. The inspectors  
the fire header because the fire pumps were able to maintain pressure in the fire header
determined the issue was of very low safety significance (Green) because the cracked  
until the ruptured valves were isolated.
fire valves were easily isolated and did not pass sufficient water to render the fire  
The inspectors determined that the finding had a cross-cutting aspect in the area of
header non-functional. Specifically, the inspectors assigned a low degradation rating to  
human performance related to work practices - human error prevention techniques.
the fire header because the fire pumps were able to maintain pressure in the fire header  
Specifically, Entergy personnel routinely tour the 11 fire pump house did not question
until the ruptured valves were isolated.
the abnormally cold room temperatures. (H.4(a) per IMC 0305)
Enforcement: Enforcement action does not apply because the performance deficiency
The inspectors determined that the finding had a cross-cutting aspect in the area of  
did not involve a violation of a regulatory requirement. Because this finding does not
human performance related to work practices - human error prevention techniques.
involve a violation of regulatory requirements and has very low safety significance, it is
Specifically, Entergy personnel routinely tour the 11 fire pump house did not question  
identified as FIN 05000247/2009002-01, Failure to Identify Open Louvers in 11 Fire
the abnormally cold room temperatures. (H.4(a) per IMC 0305)  
Pump House.
                                                                                    Enclosure
Enforcement: Enforcement action does not apply because the performance deficiency  
did not involve a violation of a regulatory requirement. Because this finding does not  
involve a violation of regulatory requirements and has very low safety significance, it is  
identified as FIN 05000247/2009002-01, Failure to Identify Open Louvers in 11 Fire  
Pump House.  


                                                10
10  
1R04 Equipment Alignment (71111.04Q - 3 samples)
Enclosure 
      Partial System Walkdowns
1R04 Equipment Alignment (71111.04Q - 3 samples)  
  a.   Inspection Scope
      The inspectors performed partial system walkdowns to verify the operability of redundant
      or diverse trains and components during periods of system train unavailability, or
Partial System Walkdowns  
      following periods of maintenance. The inspectors referenced the system procedures,
   
      the UFSAR, and system drawings to verify the alignment of the available train supported
  a.  
      its required safety functions. The inspectors also reviewed applicable condition reports
Inspection Scope  
      (CR) and work orders to ensure Entergy personnel identified and properly addressed
      equipment discrepancies that could potentially impair the capability of the available train,
The inspectors performed partial system walkdowns to verify the operability of redundant  
      as required by Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix
or diverse trains and components during periods of system train unavailability, or  
      B, Criterion XVI, Corrective Action. The documents reviewed during these inspections
following periods of maintenance. The inspectors referenced the system procedures,  
      are listed in the Attachment.
the UFSAR, and system drawings to verify the alignment of the available train supported  
      The inspectors performed a partial walkdown on the following systems, which
its required safety functions. The inspectors also reviewed applicable condition reports  
      represented three inspection samples:
(CR) and work orders to ensure Entergy personnel identified and properly addressed  
    *         21 and 22 component cooling water (CCW) system train when 23 CCW pump
equipment discrepancies that could potentially impair the capability of the available train,  
              was tagged out for maintenance;
as required by Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix  
    *         City water system as a supply to auxiliary boiler feedwater (ABFW) when the
B, Criterion XVI, Corrective Action. The documents reviewed during these inspections  
              condensate storage tank was declared inoperable due to leakage;
are listed in the Attachment.  
    *         21 and 23 ABFW trains when 22 ABFW pump was tagged out and temporary
              modifications were applied to 21 and 23 ABFW minimum flow lines.
The inspectors performed a partial walkdown on the following systems, which  
  b.   Findings
represented three inspection samples:  
      No findings of significance were identified.
1R05 Fire Protection (71111.05Q - 5 samples)
*  
  a.   Inspection Scope
21 and 22 component cooling water (CCW) system train when 23 CCW pump  
      The inspectors conducted tours of several fire areas to assess the material condition and
was tagged out for maintenance;  
      operational status of fire protection features. The inspectors verified, consistent with the
*  
      applicable administrative procedures, that: combustibles and ignition sources were
City water system as a supply to auxiliary boiler feedwater (ABFW) when the  
      adequately controlled; passive fire barriers, manual fire-fighting equipment, and
condensate storage tank was declared inoperable due to leakage;  
      suppression and detection equipment were appropriately maintained; and compensatory
*  
      measures for out-of-service, degraded, or inoperable fire protection equipment were
21 and 23 ABFW trains when 22 ABFW pump was tagged out and temporary  
      implemented in accordance with Entergys fire protection program. The inspectors
modifications were applied to 21 and 23 ABFW minimum flow lines.  
      evaluated the fire protection program for conformance with the requirements of License
   
      Condition 2.K. The documents reviewed during this inspection are listed in the
b.  
      Attachment. This inspection represented five inspection samples for fire protection
Findings  
      tours, and was conducted in the following areas:
      *       FZ 65, Main Steam/Feed Regulating Valve Areas;
      *       FZ 23, 62A Auxiliary Feed Pump Room & Building;
No findings of significance were identified.  
      *       FZ 14, 480V Vital AC Switchgear Room;
      *       FZ 10, Emergency Diesel Generator Building; and
1R05 Fire Protection (71111.05Q - 5 samples)  
      *       FZ 360, Station Blackout Diesel Area.
   
                                                                                        Enclosure
  a.  
Inspection Scope  
The inspectors conducted tours of several fire areas to assess the material condition and  
operational status of fire protection features. The inspectors verified, consistent with the  
applicable administrative procedures, that: combustibles and ignition sources were  
adequately controlled; passive fire barriers, manual fire-fighting equipment, and  
suppression and detection equipment were appropriately maintained; and compensatory  
measures for out-of-service, degraded, or inoperable fire protection equipment were  
implemented in accordance with Entergys fire protection program. The inspectors  
evaluated the fire protection program for conformance with the requirements of License  
Condition 2.K. The documents reviewed during this inspection are listed in the  
Attachment. This inspection represented five inspection samples for fire protection  
tours, and was conducted in the following areas:  
*  
FZ 65, Main Steam/Feed Regulating Valve Areas;  
*  
FZ 23, 62A Auxiliary Feed Pump Room & Building;  
*  
FZ 14, 480V Vital AC Switchgear Room;  
*  
FZ 10, Emergency Diesel Generator Building; and  
*  
FZ 360, Station Blackout Diesel Area.  


                                              11
11  
  b. Findings
Enclosure  
.1 Failure to Identify Damaged Components in EDG Ventilation Motor Control Center
b.  
    Introduction: The inspectors identified a NCV of very low safety significance (Green)
Findings  
    related to 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, because Entergy
    personnel did not promptly identify and correct an adverse condition related to an
.1  
    electrical fault. Specifically, personnel did not identify a safety-related cubicle (bucket)
Failure to Identify Damaged Components in EDG Ventilation Motor Control Center  
    had experienced a fault prior to replacement of upstream fuses and restoration of power
    to the cubicle.
Introduction: The inspectors identified a NCV of very low safety significance (Green)  
    Description: On January 28, 2009, operations personnel detected an acrid odor coming
related to 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, because Entergy  
    from the emergency diesel generator (EDG) building. Operators entered the EDG
personnel did not promptly identify and correct an adverse condition related to an  
    building to investigate the source of the acrid odor and identified that a MCC was de-
electrical fault. Specifically, personnel did not identify a safety-related cubicle (bucket)  
    energized. Operations personnel did not identify external damage to the MCC; however,
had experienced a fault prior to replacement of upstream fuses and restoration of power  
    operators did not open MCC panels to inspect for internal damage. Operators checked
to the cubicle.
    the upstream 175 amp supply fuses, located in a different building, and identified that 2
    of 3 fuses had blown. Operators opened the downstream breakers on the MCC in the
Description: On January 28, 2009, operations personnel detected an acrid odor coming  
    EDG building and then replaced the 175 amp supply fuses in the control building. Once
from the emergency diesel generator (EDG) building. Operators entered the EDG  
    operators replaced the blown fuses, they re-energized the EDG building MCC#1, and
building to investigate the source of the acrid odor and identified that a MCC was de-
    subsequently began to locally shut all of the cubicle switches. When operators
energized. Operations personnel did not identify external damage to the MCC; however,  
    attempted to shut the switch associated with cubicle 4N, the switch did not function as
operators did not open MCC panels to inspect for internal damage. Operators checked  
    expected. Operators then opened the panel for cubicle 4N and identified charred
the upstream 175 amp supply fuses, located in a different building, and identified that 2  
    electrical components.
of 3 fuses had blown. Operators opened the downstream breakers on the MCC in the  
    Entergy personnel generated a D level condition report (CR) for cubicle 4N on the
EDG building and then replaced the 175 amp supply fuses in the control building. Once  
    basis that it supplies a non safety-related (NSR) EDG room heater. Entergy personnel
operators replaced the blown fuses, they re-energized the EDG building MCC#1, and  
    closed the CR to a work request to troubleshoot and repair the NSR heater. However,
subsequently began to locally shut all of the cubicle switches. When operators  
    the inspectors questioned the classification of the MCC and determined that the charred
attempted to shut the switch associated with cubicle 4N, the switch did not function as  
    components were safety related (SR). Cubicle 4N contains a SR main line switch and
expected. Operators then opened the panel for cubicle 4N and identified charred  
    SR 30 amp main line fuses. The 30 amp fuses are SR to isolate the NSR heaters from
electrical components.
    the MCC in the event of a room heater fault. The inspectors also questioned the
    appropriateness of leaving the damaged cubicle in the energized MCC. Following
Entergy personnel generated a D level condition report (CR) for cubicle 4N on the  
    inspector questions, Entergy staff issued another CR and removed the damaged cubicle
basis that it supplies a non safety-related (NSR) EDG room heater. Entergy personnel  
    from the MCC on February 11. During removal of the charred cubicle, maintenance
closed the CR to a work request to troubleshoot and repair the NSR heater. However,  
    personnel were unable to disconnect the main line cables due to arc-welding at the
the inspectors questioned the classification of the MCC and determined that the charred  
    termination and subsequently had to cut two of the three cables upstream of the
components were safety related (SR). Cubicle 4N contains a SR main line switch and  
    termination and cubicle switch. These cables and the line side of the switch were
SR 30 amp main line fuses. The 30 amp fuses are SR to isolate the NSR heaters from  
    energized from January 28 until February 11. After the damaged cubicle was removed,
the MCC in the event of a room heater fault. The inspectors also questioned the  
    engineering personnel performed an inspection and determined that the fault originated
appropriateness of leaving the damaged cubicle in the energized MCC. Following  
    from a high resistance connection on the C phase between the main fuse clip and the
inspector questions, Entergy staff issued another CR and removed the damaged cubicle  
    cubicle supply switch in the 4N cubicle.
from the MCC on February 11. During removal of the charred cubicle, maintenance  
    The inspectors determined that replacing the upstream 175 Amp fuses on and restoring
personnel were unable to disconnect the main line cables due to arc-welding at the  
    power to the EDG ventilation MCC #1, which contained the charred 4N cubicle, without
termination and subsequently had to cut two of the three cables upstream of the  
    identifying the source of the acrid odor could have reinitiated the fault and increased the
termination and cubicle switch. These cables and the line side of the switch were  
    probability of a fire. In addition, operations personnel tried to locally close the damaged
energized from January 28 until February 11. After the damaged cubicle was removed,  
    switch which could have also re-initiated the fault. Entergy staff also did not take action
engineering personnel performed an inspection and determined that the fault originated  
    to remove or de-energize the charred cubicle after the condition was identified on
from a high resistance connection on the C phase between the main fuse clip and the  
    January 28, 2009. The damaged cubicle was de-energized and removed from the MCC
cubicle supply switch in the 4N cubicle.  
    on February 11 in response to the inspectors questions.
                                                                                        Enclosure
The inspectors determined that replacing the upstream 175 Amp fuses on and restoring  
power to the EDG ventilation MCC #1, which contained the charred 4N cubicle, without  
identifying the source of the acrid odor could have reinitiated the fault and increased the  
probability of a fire. In addition, operations personnel tried to locally close the damaged  
switch which could have also re-initiated the fault. Entergy staff also did not take action  
to remove or de-energize the charred cubicle after the condition was identified on  
January 28, 2009. The damaged cubicle was de-energized and removed from the MCC  
on February 11 in response to the inspectors questions.  


                                            12
12  
This issue was reasonable for the licensee to foresee and correct because acrid odor is
Enclosure 
an indication of a fault. It was reasonable for Entergy personnel to open panel doors
This issue was reasonable for the licensee to foresee and correct because acrid odor is  
and perform visual inspections of the affected MCC prior to replacing upstream fuses
an indication of a fault. It was reasonable for Entergy personnel to open panel doors  
and restoring power to the fault. The inspectors determined that the National Electrical
and perform visual inspections of the affected MCC prior to replacing upstream fuses  
Code NFPA 70E, Standard for Electrical Safety in the Workplace, prohibits
and restoring power to the fault. The inspectors determined that the National Electrical  
reenergizing a circuit after a protective device has operated until it has been determined
Code NFPA 70E, Standard for Electrical Safety in the Workplace, prohibits  
that the automatic operation was a result of an overload and not a fault. The acrid odor
reenergizing a circuit after a protective device has operated until it has been determined  
in the EDG building was an indication of a fault vice an overload condition. In addition,
that the automatic operation was a result of an overload and not a fault. The acrid odor  
once Entergy personnel identified the cubicle was charred and experienced an electrical
in the EDG building was an indication of a fault vice an overload condition. In addition,  
fault, industry standards would have operators immediately secure power and/or
once Entergy personnel identified the cubicle was charred and experienced an electrical  
remove the damaged gear from the MCC.
fault, industry standards would have operators immediately secure power and/or  
Entergy entered the issue into the corrective action program as IP2-2009-00342 and
remove the damaged gear from the MCC.  
IP2-2009-00483, trained all operations personnel on the requirements to replace fuses
and re-energize electrical equipment, and plans to review operations procedures for
Entergy entered the issue into the corrective action program as IP2-2009-00342 and  
operating electrical equipment.
IP2-2009-00483, trained all operations personnel on the requirements to replace fuses  
Analysis: The inspectors determined that Entergys failure to promptly identify an
and re-energize electrical equipment, and plans to review operations procedures for  
adverse condition associated with damaged electrical components constituted a
operating electrical equipment.
performance deficiency. This issue was more than minor because the finding was
associated with the external factors attribute of the Initiating Events cornerstone and
Analysis: The inspectors determined that Entergys failure to promptly identify an  
impacted the cornerstone objective of limiting the likelihood of those events that upset
adverse condition associated with damaged electrical components constituted a  
plant stability and challenge critical safety systems during shutdown as well as power
performance deficiency. This issue was more than minor because the finding was  
operations. Specifically, operations personnel did not identify the source of the acrid
associated with the external factors attribute of the Initiating Events cornerstone and  
odor, indicative of an electrical fault, in the EDG building; re-energized damaged
impacted the cornerstone objective of limiting the likelihood of those events that upset  
electrical equipment; and left damaged electrical components (cubicle 4N) energized for
plant stability and challenge critical safety systems during shutdown as well as power  
14 days prior to its removal from the MCC. The inspectors determined these issues
operations. Specifically, operations personnel did not identify the source of the acrid  
increased the likelihood of a fire in the EDG building. The condition was evaluated by a
odor, indicative of an electrical fault, in the EDG building; re-energized damaged  
Senior Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection
electrical equipment; and left damaged electrical components (cubicle 4N) energized for  
Significance Determination Process. It was determined that in the event of a fire
14 days prior to its removal from the MCC. The inspectors determined these issues  
consuming the MCC, no transient would be placed on the plant and no components
increased the likelihood of a fire in the EDG building. The condition was evaluated by a  
required to safely shutdown the plant would be impacted. As a result, in accordance
Senior Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection  
with task 2.3.5 of Appendix F, the issue was screened to Green.
Significance Determination Process. It was determined that in the event of a fire  
The inspectors determined that a cross-cutting aspect was associated with this finding
consuming the MCC, no transient would be placed on the plant and no components  
in the area of human performance related to conservative decision making. Specifically,
required to safely shutdown the plant would be impacted. As a result, in accordance  
Entergys decision-making was non-conservative as it related to the processes used to
with task 2.3.5 of Appendix F, the issue was screened to Green.  
identify the source of the acrid odor; re-energize the damaged electrical equipment; and
keep a damaged electrical component energized for 14 days prior to its removal from
The inspectors determined that a cross-cutting aspect was associated with this finding  
the MCC. (H.1(b) per IMC 0305)
in the area of human performance related to conservative decision making. Specifically,  
Enforcement: 10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires that
Entergys decision-making was non-conservative as it related to the processes used to  
measures shall be established to assure conditions adverse to quality, such as failures
identify the source of the acrid odor; re-energize the damaged electrical equipment; and  
and malfunctions are promptly identified and corrected. Contrary to the above, on
keep a damaged electrical component energized for 14 days prior to its removal from  
January 28, 2009, operations personnel did not identify that a safety-related bucket had
the MCC. (H.1(b) per IMC 0305)
experienced a fault prior to replacing upstream fuses and restoring power to the bucket.
In addition, after replacing the upstream fuses, operations personnel tried to locally shut
Enforcement: 10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires that  
the damaged cubicle switch and left damaged equipment energized until February 11,
measures shall be established to assure conditions adverse to quality, such as failures  
2009. Entergy entered the issue into the corrective action program as IP2-2009-00342
and malfunctions are promptly identified and corrected. Contrary to the above, on  
and IP2-2009-00483, trained all operations personnel on the requirements to replace
January 28, 2009, operations personnel did not identify that a safety-related bucket had  
fuses and re-energize electrical equipment, and plans to review operations procedures
experienced a fault prior to replacing upstream fuses and restoring power to the bucket.  
                                                                                  Enclosure
In addition, after replacing the upstream fuses, operations personnel tried to locally shut  
the damaged cubicle switch and left damaged equipment energized until February 11,  
2009. Entergy entered the issue into the corrective action program as IP2-2009-00342  
and IP2-2009-00483, trained all operations personnel on the requirements to replace  
fuses and re-energize electrical equipment, and plans to review operations procedures  


                                            13
13  
  for operating electrical equipment. Because the violation was of very low safety
Enclosure 
  significance and it was entered into the licensees corrective action program, this
for operating electrical equipment. Because the violation was of very low safety  
  violation is being treated as an NCV, consistent with the NRC Enforcement Policy: NCV
significance and it was entered into the licensees corrective action program, this  
  05000247/2009002-02, Failure to Identify Damaged Components in EDG
violation is being treated as an NCV, consistent with the NRC Enforcement Policy: NCV  
  Ventilation Motor Control Center.
05000247/2009002-02, Failure to Identify Damaged Components in EDG  
.2 Degraded Fire Door to the 480V Vital Bus Room
Ventilation Motor Control Center.  
  Introduction: The inspectors identified a NCV of very low safety significance (Green)
  related to License Condition 2.K., fire protection program, because Entergy personnel
.2  
  did not promptly identify and correct a degraded three-hour rated fire door on the west
Degraded Fire Door to the 480V Vital Bus Room  
  entrance of the 480 Volt switchgear room.
  Description: License Condition 2.K., fire protection program, requires that Entergy
Introduction: The inspectors identified a NCV of very low safety significance (Green)  
  implement and maintain in effect all provisions of the NRC-approved fire protection
related to License Condition 2.K., fire protection program, because Entergy personnel  
  program, as approved in part by the NRC Safety Evaluation Report (SER) dated
did not promptly identify and correct a degraded three-hour rated fire door on the west  
  January 31, 1979. The January 31, 1979, SER requires administrative controls
entrance of the 480 Volt switchgear room.
  comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for
  Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch
Description: License Condition 2.K., fire protection program, requires that Entergy  
  Technical Position (BTP) 9.5-1 requires that measures be established to assure that
implement and maintain in effect all provisions of the NRC-approved fire protection  
  conditions adverse to fire protection, such as deficiencies, deviations, defective
program, as approved in part by the NRC Safety Evaluation Report (SER) dated  
  components, and non-conformities are promptly identified, reported, and corrected.
January 31, 1979. The January 31, 1979, SER requires administrative controls  
  On February 6, 2009, the inspectors performed a fire protection walkdown of the 480-
comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for  
  Volt switchgear room. The inspectors noted the three-hour rated, swing-type fire door
Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch  
  on the west side of the 480-Volt switchgear room was not latched closed. The
Technical Position (BTP) 9.5-1 requires that measures be established to assure that  
  inspectors observed the door being held open by the latch mechanism which had not
conditions adverse to fire protection, such as deficiencies, deviations, defective  
  repositioned to allow the door to shut. The inspectors observed the latch mechanism
components, and non-conformities are promptly identified, reported, and corrected.  
  did not move freely preventing the door from shutting automatically. The inspectors
  shut the door and notified shift operations personnel who tightened latch screws on the
On February 6, 2009, the inspectors performed a fire protection walkdown of the 480-
  door and wrote a condition report.
Volt switchgear room. The inspectors noted the three-hour rated, swing-type fire door  
  On February 18, the inspectors identified the 480-Volt switchgear room door was not
on the west side of the 480-Volt switchgear room was not latched closed. The  
  latched shut again. The inspectors determined the door could not be closed due to
inspectors observed the door being held open by the latch mechanism which had not  
  interference from the latch mechanism screw which had backed out. The inspectors
repositioned to allow the door to shut. The inspectors observed the latch mechanism  
  notified operations of the fire door issue. Operations personnel re-inserted the latch
did not move freely preventing the door from shutting automatically. The inspectors  
  mechanism screw and documented the issue in a condition report. The inspectors
shut the door and notified shift operations personnel who tightened latch screws on the  
  questioned whether it was appropriate to re-insert a screw that had backed out on its
door and wrote a condition report.  
  own in such a short period of time. Entergy personnel subsequently inspected the door
  on February 23 and identified the screws holding the latch mechanism to the door were
On February 18, the inspectors identified the 480-Volt switchgear room door was not  
  stripped. Entergy personnel tapped new holes in the door latch mechanism and
latched shut again. The inspectors determined the door could not be closed due to  
  installed new screws.
interference from the latch mechanism screw which had backed out. The inspectors  
  On March 3, inspectors identified the 480-Volt switchgear room fire door not latched
notified operations of the fire door issue. Operations personnel re-inserted the latch  
  shut again. The inspectors observed the door was being held open by the latch
mechanism screw and documented the issue in a condition report. The inspectors  
  mechanism which had not repositioned to allow the door to shut. The inspectors noted
questioned whether it was appropriate to re-insert a screw that had backed out on its  
  the latch mechanism did not move freely preventing the door from shutting
own in such a short period of time. Entergy personnel subsequently inspected the door  
  automatically. The inspectors notified operations personnel of the non-functioning fire
on February 23 and identified the screws holding the latch mechanism to the door were  
  door and Entergy subsequently had a locksmith inspect the latch. The locksmith
stripped.   Entergy personnel tapped new holes in the door latch mechanism and  
  installed a new latch mechanism on March 3 and determined the latch issues observed
installed new screws.  
  were age-related due to interaction of wear products from the latch interfering with the
  moving portions of the latch, as a result of latching and unlatching door operations.
On March 3, inspectors identified the 480-Volt switchgear room fire door not latched  
                                                                                    Enclosure
shut again. The inspectors observed the door was being held open by the latch  
mechanism which had not repositioned to allow the door to shut. The inspectors noted  
the latch mechanism did not move freely preventing the door from shutting  
automatically. The inspectors notified operations personnel of the non-functioning fire  
door and Entergy subsequently had a locksmith inspect the latch. The locksmith  
installed a new latch mechanism on March 3 and determined the latch issues observed  
were age-related due to interaction of wear products from the latch interfering with the  
moving portions of the latch, as a result of latching and unlatching door operations.


                                                14
14  
      Entergy entered the issue into the corrective action program on March 3, performed an
Enclosure 
      inspection of all fire doors onsite, and identified and corrected issues with other required
Entergy entered the issue into the corrective action program on March 3, performed an  
      fire doors.
inspection of all fire doors onsite, and identified and corrected issues with other required  
      Analysis: The inspectors identified a performance deficiency because Entergy personnel
fire doors.  
      did not identify and correct the non-functional fire door. The finding was more than
      minor because it is associated with the protection against external factors attribute of
Analysis: The inspectors identified a performance deficiency because Entergy personnel  
      the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring
did not identify and correct the non-functional fire door. The finding was more than  
      the reliability of systems that respond to initiating events to prevent undesirable
minor because it is associated with the protection against external factors attribute of  
      consequences. Specifically, in the event of a large fire in the 480-Volt switchgear room
the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring  
      or the turbine building, the affected fire door is credited to prevent the spread of fire from
the reliability of systems that respond to initiating events to prevent undesirable  
      one area to the other area. This fire door, when degraded, impacts the reliability of
consequences. Specifically, in the event of a large fire in the 480-Volt switchgear room  
      mitigating systems in the 480-Volt switchgear room that are relied upon during a large
or the turbine building, the affected fire door is credited to prevent the spread of fire from  
      fire in the turbine building, and vice versa.
one area to the other area. This fire door, when degraded, impacts the reliability of  
      This finding was evaluated using Phase 1 of IMC 0609 Appendix F, Fire Protection
mitigating systems in the 480-Volt switchgear room that are relied upon during a large  
      Significance Determination Process. Since the area in question had a fire watch
fire in the turbine building, and vice versa.  
      posted during the time the door was degraded, an adequate level of protection was
      maintained to compensate for the degraded door and resulted in the finding being of
This finding was evaluated using Phase 1 of IMC 0609 Appendix F, Fire Protection  
      very low safety significance. As such according to task 1.3.1, the inspectors determined
Significance Determination Process. Since the area in question had a fire watch  
      the finding was Green.
posted during the time the door was degraded, an adequate level of protection was  
      The inspectors determined that the finding had a cross-cutting aspect in the area of
maintained to compensate for the degraded door and resulted in the finding being of  
      problem identification and resolution because Entergy personnel did not thoroughly
very low safety significance. As such according to task 1.3.1, the inspectors determined  
      evaluate a degraded fire door latch on several occasions, such that the resolution of the
the finding was Green.
      problems addressed the causes. (P.1(c) per IMC 0305)
      Enforcement: License Condition 2.K., fire protection program, requires that Entergy
The inspectors determined that the finding had a cross-cutting aspect in the area of  
      implement and maintain in effect all provisions of the NRC-approved fire protection
problem identification and resolution because Entergy personnel did not thoroughly  
      program, as approved in part by the NRC Safety Evaluation Report (SER) dated
evaluate a degraded fire door latch on several occasions, such that the resolution of the  
      January 31, 1979. The January 31, 1979, SER requires administrative controls
problems addressed the causes. (P.1(c) per IMC 0305)  
      comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for
      Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch
Enforcement: License Condition 2.K., fire protection program, requires that Entergy  
      Technical Position 9.5-1 requires that measures be established to assure that conditions
implement and maintain in effect all provisions of the NRC-approved fire protection  
      adverse to fire protection, such as deficiencies, deviations, defective components, and
program, as approved in part by the NRC Safety Evaluation Report (SER) dated  
      non-conformities are promptly identified, reported, and corrected.
January 31, 1979. The January 31, 1979, SER requires administrative controls  
      Contrary to the above, Entergy personnel did not promptly identify and then
comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for  
      subsequently correct the non-functional 480-Volt switchgear fire door. This fire door
Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch  
      was identified by inspectors in a non-functional state on February 6, February 18, and
Technical Position 9.5-1 requires that measures be established to assure that conditions  
      again on March 3, 2009. Entergy entered the issue into the corrective action program
adverse to fire protection, such as deficiencies, deviations, defective components, and  
      as IP2-2009-00526, IP2-2009-00680, IP2-2009-00709, IP2-2009-00834, IP2-2009-
non-conformities are promptly identified, reported, and corrected.  
      00842, and IP2-2009-00843. Because the violation was of very low safety significance
      and it was entered into the licensees corrective action program, this violation is being
Contrary to the above, Entergy personnel did not promptly identify and then  
      treated as an NCV, consistent with the NRC Enforcement Policy: NCV
subsequently correct the non-functional 480-Volt switchgear fire door. This fire door  
      05000247/2009002-03, Failure to Identify and Promptly Correct Degraded 480-Volt
was identified by inspectors in a non-functional state on February 6, February 18, and  
      Switchgear Room Fire Door.
again on March 3, 2009. Entergy entered the issue into the corrective action program  
1R07 Heat Sink Performance (71111.07A - 1 sample)
as IP2-2009-00526, IP2-2009-00680, IP2-2009-00709, IP2-2009-00834, IP2-2009-
  a. Inspection Scope
00842, and IP2-2009-00843. Because the violation was of very low safety significance  
                                                                                        Enclosure
and it was entered into the licensees corrective action program, this violation is being  
treated as an NCV, consistent with the NRC Enforcement Policy: NCV  
05000247/2009002-03, Failure to Identify and Promptly Correct Degraded 480-Volt  
Switchgear Room Fire Door.  
1R07 Heat Sink Performance (71111.07A - 1 sample)  
   
  a.  
Inspection Scope  


                                                15
15  
      The inspectors selected the 22 component water heat exchanger for review to
Enclosure 
      determine the heat exchangers readiness and availability to perform its safety functions.
      The inspectors reviewed the design basis for the component, reviewed Entergy
      commitments to NRC Generic Letter 89-13, and reviewed engineering reports that
      documented results of previous internal inspections. The inspectors also observed the
The inspectors selected the 22 component water heat exchanger for review to  
      disassembly, inspection, and cleaning of the heat exchanger and reviewed engineering
determine the heat exchangers readiness and availability to perform its safety functions.
      results of the inspection to verify that appropriate corrective actions were initiated for
The inspectors reviewed the design basis for the component, reviewed Entergy  
      deficiencies that were discovered. The inspectors reviewed documents for and verified
commitments to NRC Generic Letter 89-13, and reviewed engineering reports that  
      that the amount of tubes plugged within the heat exchanger did not exceed the
documented results of previous internal inspections. The inspectors also observed the  
      maximum amount allowed. Documents reviewed are listed in the appendix.
disassembly, inspection, and cleaning of the heat exchanger and reviewed engineering  
  b.  Findings
results of the inspection to verify that appropriate corrective actions were initiated for  
    No findings of significance were identified.
deficiencies that were discovered. The inspectors reviewed documents for and verified  
1R11 Licensed Operator Requalification Program
that the amount of tubes plugged within the heat exchanger did not exceed the  
    Quarterly Review (71111.11Q - 1 sample)
maximum amount allowed. Documents reviewed are listed in the appendix.  
  a. Inspection Scope
   
    On February 23, 2009, the inspectors observed licensed operator simulator training
  b.  
    associated with a sustained loss of all alternating current (AC) power scenario, to verify
Findings
    that operator performance was adequate, and that evaluators were identifying and
    documenting crew performance problems. The inspectors evaluated the performance of
   
    risk-significant operator actions, including the use of emergency operating procedures.
No findings of significance were identified.  
    The inspectors assessed the clarity and effectiveness of communications, the
    implementation of appropriate actions in response to alarms, the performance of timely
1R11 Licensed Operator Requalification Program  
    control board operation and manipulation, and the oversight and direction provided by
    the control room supervisor. The inspectors also reviewed simulator fidelity with respect
Quarterly Review (71111.11Q - 1 sample)  
    to the actual plant. The inspectors evaluated licensed operator training for conformance
   
    with the requirements of 10 CFR Part 55, Operator Licenses. The documents
  a.  
    reviewed during this inspection are listed in the Attachment. This observation of
Inspection Scope  
    operator simulator training represented one inspection sample.
  b.  Findings
    No findings of significance were identified.
On February 23, 2009, the inspectors observed licensed operator simulator training  
1R12 Maintenance Effectiveness (71111.12Q - 3 samples)
associated with a sustained loss of all alternating current (AC) power scenario, to verify  
  a. Inspection Scope
that operator performance was adequate, and that evaluators were identifying and  
      The inspectors reviewed performance-based problems that involved structures,
documenting crew performance problems. The inspectors evaluated the performance of  
      systems, and components (SSCs) to assess the effectiveness of maintenance activities.
risk-significant operator actions, including the use of emergency operating procedures.
      When applicable, the reviews focused on:
The inspectors assessed the clarity and effectiveness of communications, the  
        *   Proper Maintenance Rule scoping in accordance with 10 CFR 50.65;
implementation of appropriate actions in response to alarms, the performance of timely  
        *   Characterization of reliability issues;
control board operation and manipulation, and the oversight and direction provided by  
        *   Changing system and component unavailability;
the control room supervisor. The inspectors also reviewed simulator fidelity with respect  
                                                                                          Enclosure
to the actual plant. The inspectors evaluated licensed operator training for conformance  
with the requirements of 10 CFR Part 55, Operator Licenses. The documents  
reviewed during this inspection are listed in the Attachment. This observation of  
operator simulator training represented one inspection sample.  
   
  b.  
Findings
   
No findings of significance were identified.  
1R12 Maintenance Effectiveness (71111.12Q - 3 samples)  
   
a.  
Inspection Scope  
The inspectors reviewed performance-based problems that involved structures,  
systems, and components (SSCs) to assess the effectiveness of maintenance activities.  
When applicable, the reviews focused on:  
*  
Proper Maintenance Rule scoping in accordance with 10 CFR 50.65;  
*  
Characterization of reliability issues;  
*  
Changing system and component unavailability;  


                                            16
16  
      *   10 CFR 50.65(a)(1) and (a)(2) classifications;
Enclosure 
      *   Identifying and addressing common cause failures;
*  
      *   Trending of system flow and temperature values;
10 CFR 50.65(a)(1) and (a)(2) classifications;  
      *   Appropriateness of performance criteria for SSCs classified (a)(2); and
*  
      *   Adequacy of goals and corrective actions for SSCs classified (a)(1).
Identifying and addressing common cause failures;  
  The inspectors also reviewed system health reports, maintenance backlogs, and
*  
  Maintenance Rule basis documents. The inspectors evaluated maintenance
Trending of system flow and temperature values;  
  effectiveness and monitoring activities against the requirements of 10 CFR 50.65. The
*  
  documents reviewed during this inspection are listed in the Attachment. The following
Appropriateness of performance criteria for SSCs classified (a)(2); and  
  Maintenance Rule samples were reviewed and represented three inspection samples:
*  
  *   RWST level indication system;
Adequacy of goals and corrective actions for SSCs classified (a)(1).  
  *   EDG fuel injection system; and
  *   480-Volt switchgear system.
The inspectors also reviewed system health reports, maintenance backlogs, and  
b. Findings
Maintenance Rule basis documents. The inspectors evaluated maintenance  
  Introduction: The inspectors identified a NCV of very low safety significance (Green)
effectiveness and monitoring activities against the requirements of 10 CFR 50.65. The  
  related to TS 5.4.1, Administrative Controls: Procedures, because Entergy did not
documents reviewed during this inspection are listed in the Attachment. The following  
  maintain an adequate maintenance procedure for a safety-related electrical motor
Maintenance Rule samples were reviewed and represented three inspection samples:  
  control center (MCC). Specifically, the eight-year maintenance procedure for the
  affected EDG ventilation MCC did not contain an adequate method to identify high
*  
  resistance connections within the cubicle.
RWST level indication system;  
  Description: On January 28, 2009, operations personnel identified an acrid odor coming
*  
  from the EDG building. Subsequent personnel investigation revealed a charred cubicle
EDG fuel injection system; and  
  in a safety-related 480-Volt MCC. Specifically, cubicle 4N, in the EDG ventilation MCC,
*  
  experienced a phase-to-phase fault that caused the upstream 175 amp fuses to open
480-Volt switchgear system.  
  and de-energize the MCC. Entergy personnel subsequently generated a condition
  report (CR) that was closed to a work request to troubleshoot and repair the cubicle.
  b.  
  Entergy personnel removed the damaged cubicle from the MCC on February 6 and
Findings  
  determined the likely cause to be a high-resistance connection between the cubicle
  switch and 30 amp fuse clip on the C phase resulting in long-term overheating. This
Introduction: The inspectors identified a NCV of very low safety significance (Green)  
  overheating condition degraded the insulation between two of the three phases over
related to TS 5.4.1, Administrative Controls: Procedures, because Entergy did not  
  time and eventually resulted in a phase-to-phase fault on January 28, 2009.
maintain an adequate maintenance procedure for a safety-related electrical motor  
  The inspectors reviewed the 8-year maintenance procedure 2-MCC-003-ELC,
control center (MCC). Specifically, the eight-year maintenance procedure for the  
  Klockner-Moeller, Series 200, 480 Volt Motor Control Center Preventive Maintenance,
affected EDG ventilation MCC did not contain an adequate method to identify high  
  which was performed on the affected EDG ventilation MCC on April 6, 2008. The
resistance connections within the cubicle.  
  inspectors noted that the procedure was revised the same day to allow performance of
  the maintenance without de-energizing the equipment. The revision resulted in portions
Description: On January 28, 2009, operations personnel identified an acrid odor coming  
  of the cubicle cleaning and inspection procedure not being performed because they
from the EDG building. Subsequent personnel investigation revealed a charred cubicle  
  could not be safely performed while the cubicle was energized. The inspectors
in a safety-related 480-Volt MCC. Specifically, cubicle 4N, in the EDG ventilation MCC,  
  determined that the procedure revision on April 6, 2008, was inappropriately treated as
experienced a phase-to-phase fault that caused the upstream 175 amp fuses to open  
  an editorial revision without a technical evaluation of the change performed. In addition,
and de-energize the MCC. Entergy personnel subsequently generated a condition  
  following interviews with Entergy personnel, it was determined that maintenance had not
report (CR) that was closed to a work request to troubleshoot and repair the cubicle.  
  been performed on this MCC prior to April 6, 2008.
                                                                                  Enclosure
Entergy personnel removed the damaged cubicle from the MCC on February 6 and  
determined the likely cause to be a high-resistance connection between the cubicle  
switch and 30 amp fuse clip on the C phase resulting in long-term overheating. This  
overheating condition degraded the insulation between two of the three phases over  
time and eventually resulted in a phase-to-phase fault on January 28, 2009.
The inspectors reviewed the 8-year maintenance procedure 2-MCC-003-ELC,  
Klockner-Moeller, Series 200, 480 Volt Motor Control Center Preventive Maintenance,  
which was performed on the affected EDG ventilation MCC on April 6, 2008. The  
inspectors noted that the procedure was revised the same day to allow performance of  
the maintenance without de-energizing the equipment. The revision resulted in portions  
of the cubicle cleaning and inspection procedure not being performed because they  
could not be safely performed while the cubicle was energized. The inspectors  
determined that the procedure revision on April 6, 2008, was inappropriately treated as  
an editorial revision without a technical evaluation of the change performed. In addition,  
following interviews with Entergy personnel, it was determined that maintenance had not  
been performed on this MCC prior to April 6, 2008.


                                          17
17  
The inspectors reviewed industry guidance for performing switchgear maintenance and
Enclosure 
determined that Entergy did not include standard maintenance practices typically
The inspectors reviewed industry guidance for performing switchgear maintenance and  
utilized by its staff that would have identified a high resistance connection in the cubicle.
determined that Entergy did not include standard maintenance practices typically  
Specifically, continuity checks across contacts and switches were not performed, fuse
utilized by its staff that would have identified a high resistance connection in the cubicle.
clip tensions and tightness were not performed, and all terminations could not be
Specifically, continuity checks across contacts and switches were not performed, fuse  
checked due to the decision to perform the maintenance with portions of the cubicle
clip tensions and tightness were not performed, and all terminations could not be  
energized. In addition, the inspectors determined the EDG ventilation MCCs were not
checked due to the decision to perform the maintenance with portions of the cubicle  
included in Entergys thermography program, contrary to Entergy corporate preventive
energized. In addition, the inspectors determined the EDG ventilation MCCs were not  
maintenance templates. The inspectors determined that not performing thermography
included in Entergys thermography program, contrary to Entergy corporate preventive  
on the EDG ventilation MCC constituted a missed opportunity to identify the high
maintenance templates. The inspectors determined that not performing thermography  
resistance condition.
on the EDG ventilation MCC constituted a missed opportunity to identify the high  
It is reasonable to consider the high resistance connection existed during the
resistance condition.  
maintenance performed on April 6, 2008, because high resistance connections do not
develop into phase-to-phase faults over a short period of time. This is an underlying
It is reasonable to consider the high resistance connection existed during the  
assumption for performing switchgear maintenance, which is intended to identify and
maintenance performed on April 6, 2008, because high resistance connections do not  
correct loose/high resistance connections, on an eight-year periodicity. In addition,
develop into phase-to-phase faults over a short period of time. This is an underlying  
Entergys corporate template for switchgear maintenance recommends a six-year
assumption for performing switchgear maintenance, which is intended to identify and  
periodicity and thermography every year. It is reasonable to expect Entergy to be aware
correct loose/high resistance connections, on an eight-year periodicity. In addition,  
of the existing industry guidance as well as the Entergy corporate maintenance
Entergys corporate template for switchgear maintenance recommends a six-year  
templates.
periodicity and thermography every year. It is reasonable to expect Entergy to be aware  
Entergy entered the issue into the CAP as IP2-2009-00342 and IP2-2009-00483,
of the existing industry guidance as well as the Entergy corporate maintenance  
scoped the EDG ventilation MCC into the existing thermography program, performed an
templates.  
extent-of-condition review that identified 21 additional panels that should be in the
thermography program, and plans to revise the maintenance procedure.
Entergy entered the issue into the CAP as IP2-2009-00342 and IP2-2009-00483,  
Analysis: The inspectors identified a performance deficiency because Entergy did not
scoped the EDG ventilation MCC into the existing thermography program, performed an  
maintain an adequate maintenance procedure for the safety-related EDG ventilation
extent-of-condition review that identified 21 additional panels that should be in the  
MCC. This issue was more than minor because the finding was associated with the
thermography program, and plans to revise the maintenance procedure.  
external factors attribute of the Initiating Events cornerstone and impacted the initiating
events cornerstone objective of limiting the likelihood of those events that upset plant
Analysis: The inspectors identified a performance deficiency because Entergy did not  
stability and challenge critical safety systems during shutdown as well as power
maintain an adequate maintenance procedure for the safety-related EDG ventilation  
operations. Specifically, the high resistance connection degraded into a phase-to-phase
MCC. This issue was more than minor because the finding was associated with the  
fault and increased the likelihood of a fire in the EDG building. The condition was
external factors attribute of the Initiating Events cornerstone and impacted the initiating  
evaluated by a Senior Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire
events cornerstone objective of limiting the likelihood of those events that upset plant  
Protection Significance Determination Process. It was determined that in the event of a
stability and challenge critical safety systems during shutdown as well as power  
fire consuming the MCC, no transient would be placed on the plant and no components
operations. Specifically, the high resistance connection degraded into a phase-to-phase  
required to safely shutdown the plant would be impacted. As a result, in accordance
fault and increased the likelihood of a fire in the EDG building. The condition was  
with task 2.3.5 of Appendix F, the issue was screened to Green.
evaluated by a Senior Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire  
The inspectors determined that the finding had a cross-cutting aspect associated with
Protection Significance Determination Process. It was determined that in the event of a  
the area of problem identification and resolution related to the use of operating
fire consuming the MCC, no transient would be placed on the plant and no components  
experience (OE). Specifically, Entergy personnel did not implement industry
required to safely shutdown the plant would be impacted. As a result, in accordance  
recommended practices, or an alternate equivalent method, for identifying high
with task 2.3.5 of Appendix F, the issue was screened to Green.  
resistance connections in electrical switchgear. (P.2(b) per IMC 0305)
Enforcement. TS 5.4.1 Administrative Controls: Procedures, states, Written
The inspectors determined that the finding had a cross-cutting aspect associated with  
procedures shall be established, implemented, and maintained covering the
the area of problem identification and resolution related to the use of operating  
requirements and recommendations of Appendix A of Regulatory Guide (RG) 1.33,
experience (OE). Specifically, Entergy personnel did not implement industry  
Revision 2. Appendix A of RG 1.33 requires procedures for maintenance activities that
recommended practices, or an alternate equivalent method, for identifying high  
                                                                                  Enclosure
resistance connections in electrical switchgear. (P.2(b) per IMC 0305)  
Enforcement. TS 5.4.1 Administrative Controls: Procedures, states, Written  
procedures shall be established, implemented, and maintained covering the  
requirements and recommendations of Appendix A of Regulatory Guide (RG) 1.33,  
Revision 2. Appendix A of RG 1.33 requires procedures for maintenance activities that  


                                              18
18  
      can affect the performance of safety related equipment. Contrary to the above, Entergy
Enclosure 
      did not maintain a maintenance procedure for a safety-related MCC cubicle.
can affect the performance of safety related equipment. Contrary to the above, Entergy  
      Specifically, the eight-year maintenance procedure, first performed on April 6, 2008, did
did not maintain a maintenance procedure for a safety-related MCC cubicle.  
      not contain an adequate method to identify and correct high resistance connections in
Specifically, the eight-year maintenance procedure, first performed on April 6, 2008, did  
      the cubicle. Entergy entered the issue into the CAP as IP2-2009-00342 and IP2-2009-
not contain an adequate method to identify and correct high resistance connections in  
      00483. Because the violation was of very low safety significance and it was entered into
the cubicle. Entergy entered the issue into the CAP as IP2-2009-00342 and IP2-2009-
      the licensees corrective action program, this violation is being treated as an NCV,
00483. Because the violation was of very low safety significance and it was entered into  
      consistent with the NRC Enforcement Policy: NCV 05000247/2009002-04, Inadequate
the licensees corrective action program, this violation is being treated as an NCV,  
      Maintenance Procedure for EDG Ventilation Motor Control Center.
consistent with the NRC Enforcement Policy: NCV 05000247/2009002-04, Inadequate  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 6 samples)
Maintenance Procedure for EDG Ventilation Motor Control Center.  
  a. Inspection Scope
    The inspectors reviewed scheduled and emergent maintenance activities to verify the
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 6 samples)  
    appropriate risk assessments were performed prior to removing equipment from service
   
    for maintenance or repair. The inspectors verified that risk assessments were performed
  a.  
    as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent
Inspection Scope  
    work was performed, the inspectors verified the plant risk was promptly reassessed and
    managed. Documents reviewed during this inspection are listed in the Attachment. The
    following activities represented six inspection samples:
The inspectors reviewed scheduled and emergent maintenance activities to verify the  
    *   Emergent maintenance on the 22 EDG lube oil pump during the 23 EDG
appropriate risk assessments were performed prior to removing equipment from service  
          maintenance outage;
for maintenance or repair. The inspectors verified that risk assessments were performed  
    *   Planned risk during 21 auxiliary boiler feedwater (ABFW) pump outage and reactor
as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent  
          protection system testing;
work was performed, the inspectors verified the plant risk was promptly reassessed and  
    *   Unplanned elevated risk condition due to delayed work on reactor protection system
managed. Documents reviewed during this inspection are listed in the Attachment. The  
          components during planned maintenance of 22 ABFW pump;
following activities represented six inspection samples:  
    *   Planned maintenance on a reactor water storage tank level indicator;
    *   Planned maintenance on the 22 ABFW pump while temporary modifications were
*  
          applied to the 21 and 23 ABFW pumps; and
Emergent maintenance on the 22 EDG lube oil pump during the 23 EDG  
    *   Planned risk during 23 EDG testing and maintenance.
maintenance outage;  
  b.  Findings
*  
    Introduction: The inspectors identified a NCV of very low safety significance (Green)
Planned risk during 21 auxiliary boiler feedwater (ABFW) pump outage and reactor  
    related to 10 CFR 50.65(a)(4) because Entergy staff did not adequately assess the risk
protection system testing;  
    associated with the unavailability of the Refueling Water Storage Tank (RWST) level
*  
    indication during planned maintenance on the level transmitters and instrumentation.
Unplanned elevated risk condition due to delayed work on reactor protection system  
    Description: On February 6, 2009, Entergy staff performed maintenance on the RWST
components during planned maintenance of 22 ABFW pump;  
    level indication system. The inspectors identified that the online risk assessment did not
*  
    consider planned maintenance on the RWST level indication, as required by 10 CFR
Planned maintenance on a reactor water storage tank level indicator;  
    50.65(a)(4). The inspectors reviewed the work activity and noted the maintenance
*  
    scheduling software used by Entergy did not have the RWST maintenance coded as a
Planned maintenance on the 22 ABFW pump while temporary modifications were  
    risk-significant activity. Entergys maintenance planning process prompts the
applied to the 21 and 23 ABFW pumps; and  
    organization to evaluate the risk impact of all maintenance activities coded as risk-
*  
    significant. Therefore, a risk assessment was not performed for the quarterly RWST
Planned risk during 23 EDG testing and maintenance.
    level indication maintenance as required. In addition, the RWST level indication was not
   
    represented in Entergys interactive risk model. Entergy staff subsequently updated the
  b.  
    risk model to include the RWST level indication and subsequently assessed the online
Findings
                                                                                      Enclosure
   
Introduction: The inspectors identified a NCV of very low safety significance (Green)  
related to 10 CFR 50.65(a)(4) because Entergy staff did not adequately assess the risk  
associated with the unavailability of the Refueling Water Storage Tank (RWST) level  
indication during planned maintenance on the level transmitters and instrumentation.
Description: On February 6, 2009, Entergy staff performed maintenance on the RWST  
level indication system. The inspectors identified that the online risk assessment did not  
consider planned maintenance on the RWST level indication, as required by 10 CFR  
50.65(a)(4). The inspectors reviewed the work activity and noted the maintenance  
scheduling software used by Entergy did not have the RWST maintenance coded as a  
risk-significant activity. Entergys maintenance planning process prompts the  
organization to evaluate the risk impact of all maintenance activities coded as risk-
significant. Therefore, a risk assessment was not performed for the quarterly RWST  
level indication maintenance as required. In addition, the RWST level indication was not  
represented in Entergys interactive risk model. Entergy staff subsequently updated the  
risk model to include the RWST level indication and subsequently assessed the online  


                                              19
19  
    risk for the maintenance which resulted in a measurable increase in the core damage
Enclosure 
    frequency (CDF). The increase in CDF was not large enough to require entrance into
risk for the maintenance which resulted in a measurable increase in the core damage  
    the higher risk category per Entergy procedures. In addition, the increase in CDF (1.1E-
frequency (CDF). The increase in CDF was not large enough to require entrance into  
    6) combined with the limited duration of the maintenance (15 hours) resulted in a
the higher risk category per Entergy procedures. In addition, the increase in CDF (1.1E-
    relatively small incremental core damage probability deficit (1.9E-9).
6) combined with the limited duration of the maintenance (15 hours) resulted in a  
    The inspectors determined this same maintenance activity is modeled in the Indian Point
relatively small incremental core damage probability deficit (1.9E-9).  
    Unit 3 risk model. Entergy entered the issue into the corrective action program (CR-IP2-
    2009-00342), updated the risk model to include the maintenance activity, assessed the
The inspectors determined this same maintenance activity is modeled in the Indian Point  
    risk, and appropriately coded the maintenance activity to ensure it would be risk
Unit 3 risk model. Entergy entered the issue into the corrective action program (CR-IP2-
    assessed in the future.
2009-00342), updated the risk model to include the maintenance activity, assessed the  
    Analysis: The inspectors identified a performance deficiency in that Entergy staff did not
risk, and appropriately coded the maintenance activity to ensure it would be risk  
    assess the increase in plant risk resulting from planned maintenance activities on RWST
assessed in the future.
    level instrumentation as required by 10 CFR 50.65(a)(4). The inspectors determined
    that this finding was more than minor because it was a risk assessment issue in which
    Entergy personnel did not consider risk significant SSCs that were unavailable during
Analysis: The inspectors identified a performance deficiency in that Entergy staff did not  
    maintenance. Specifically, RWST level indication is included in Table 2 of the plant
assess the increase in plant risk resulting from planned maintenance activities on RWST  
    specific Phase 2 SDP risk-informed inspection notebook. The inspectors assessed the
level instrumentation as required by 10 CFR 50.65(a)(4). The inspectors determined  
    significance of this issue in accordance with IMC 0609, Appendix K, Maintenance Risk
that this finding was more than minor because it was a risk assessment issue in which  
    Assessment and Risk Management Significance Determination Process. The
Entergy personnel did not consider risk significant SSCs that were unavailable during  
    inspectors determined that this finding was of very low safety significance (Green)
maintenance. Specifically, RWST level indication is included in Table 2 of the plant  
    because the incremental core damage probability deficit was less than 1E-6.
specific Phase 2 SDP risk-informed inspection notebook. The inspectors assessed the  
    The inspectors determined that the finding had a cross-cutting aspect in human
significance of this issue in accordance with IMC 0609, Appendix K, Maintenance Risk  
    performance related work control. Specifically, Entergy personnel did not appropriately
Assessment and Risk Management Significance Determination Process. The  
    plan work activities by incorporating risk insights for affected plant equipment. (H.3(a)
inspectors determined that this finding was of very low safety significance (Green)  
    per IMC 0305)
because the incremental core damage probability deficit was less than 1E-6.  
    Enforcement: 10 CFR 50.65 (a)(4) states, in part that licensees shall assess and
    manage the increase in risk that may result from the proposed maintenance activities
The inspectors determined that the finding had a cross-cutting aspect in human  
    before performing those activities. Contrary to the above, on February 6, 2009, Entergy
performance related work control. Specifically, Entergy personnel did not appropriately  
    performed maintenance on the RWST level indication system without assessing the
plan work activities by incorporating risk insights for affected plant equipment. (H.3(a)  
    increase in risk. Entergy entered the issue into the corrective action program (CR-IP2-
per IMC 0305)  
    2009-00342. Because this issue is of very low safety significance and is entered into
    Entergys corrective action program, this violation is being treated as an NCV consistent
Enforcement: 10 CFR 50.65 (a)(4) states, in part that licensees shall assess and  
    the NRC Enforcement Policy: NCV 05000247/2009002-05, Failure to Include RWST
manage the increase in risk that may result from the proposed maintenance activities  
    Level Maintenance In Online Risk Assessment.
before performing those activities. Contrary to the above, on February 6, 2009, Entergy  
1R15 Operability Evaluations (71111.15 - 7 samples)
performed maintenance on the RWST level indication system without assessing the  
a.   Inspection Scope
increase in risk. Entergy entered the issue into the corrective action program (CR-IP2-
    The inspectors reviewed operability evaluations to assess the acceptability of the
2009-00342. Because this issue is of very low safety significance and is entered into  
    evaluations, the use and control of compensatory measures when applicable, and
Entergys corrective action program, this violation is being treated as an NCV consistent  
    compliance with Technical Specifications. The inspectors reviews included verification
the NRC Enforcement Policy: NCV 05000247/2009002-05, Failure to Include RWST  
    that operability determinations were performed in accordance with procedure
Level Maintenance In Online Risk Assessment.  
    ENN-OP-104, Operability Determinations. The inspectors assessed the technical
    adequacy of the evaluations to ensure consistency with the Technical Specifications,
1R15 Operability Evaluations (71111.15 - 7 samples)  
    UFSAR, and associated design basis documents. The documents reviewed are listed in
                                                                                      Enclosure
a.  
Inspection Scope  
The inspectors reviewed operability evaluations to assess the acceptability of the  
evaluations, the use and control of compensatory measures when applicable, and  
compliance with Technical Specifications. The inspectors reviews included verification  
that operability determinations were performed in accordance with procedure  
ENN-OP-104, Operability Determinations. The inspectors assessed the technical  
adequacy of the evaluations to ensure consistency with the Technical Specifications,  
UFSAR, and associated design basis documents. The documents reviewed are listed in  


                                                  20
20  
    the Attachment. The following operability evaluations were reviewed and represented
Enclosure 
    seven inspection samples:
the Attachment. The following operability evaluations were reviewed and represented  
    *   Proximity of 480-Volt vital motor control center to an uninsulated steam line;
seven inspection samples:  
    *   Leakage from condensate storage tank (CST) return piping;
    *     Impacts of scaffolding built in the vicinity of the 21 and 22 component cooling water
*  
          heat exchangers;
Proximity of 480-Volt vital motor control center to an uninsulated steam line;  
    *     Impact on pressurizer surge line and reactor coolant system piping while performing
*  
          reactor plant startups and shutdowns due to thermal transients;
Leakage from condensate storage tank (CST) return piping;  
    *     Performance impact on the 21 and 22 auxiliary component cooling pumps (ACCPs)
*  
          with respect to a potential hydraulic lock-out condition of the 21 ACCP due to 22
Impacts of scaffolding built in the vicinity of the 21 and 22 component cooling water  
          ACCP larger impeller size;
heat exchangers;  
    *   Mechanical failure of a grease fitting on 21 service water pump; and
*  
    *   Low temperatures in condensate storage tank volume.
Impact on pressurizer surge line and reactor coolant system piping while performing  
b.   Findings
reactor plant startups and shutdowns due to thermal transients;  
      No findings of significance were identified. With respect to the CST return piping, the
*  
      inspectors determined Entergy operators maintained the CST aligned to supply water to
Performance impact on the 21 and 22 auxiliary component cooling pumps (ACCPs)  
      the AFW pumps. The inspectors concluded the leakage did not prevent the CST from
with respect to a potential hydraulic lock-out condition of the 21 ACCP due to 22  
      fulfilling its safety function. Specifically, design features of the CST and the elevation of
ACCP larger impeller size;  
      the return line relative to the leak location provided assurance that, in the event the CST
*  
      return line leak increased significantly, the CST water volume would have been
Mechanical failure of a grease fitting on 21 service water pump; and  
      maintained above TS minimum required water level and able to supply the required
*  
      water to the auxiliary feedwater system.
Low temperatures in condensate storage tank volume.  
1R18 Plant Modifications (71111.18 - 2 samples)
.1   Temporary Modifications
b.  
a. Inspection Scope
Findings  
    The inspectors reviewed one temporary plant modification package for securing
    minimum flow lines on the motor driven auxiliary boiler feedwater pumps (ABFPs) and
    controlling the operation on the ABFPs through a temporary operating procedure during
No findings of significance were identified. With respect to the CST return piping, the  
    repairs of the CST return piping. The inspectors verified the design bases, licensing
inspectors determined Entergy operators maintained the CST aligned to supply water to  
    bases, and performance capability of the system was not degraded by the temporary
the AFW pumps. The inspectors concluded the leakage did not prevent the CST from  
    modification. The inspectors review included Entergys engineering evaluation for
fulfilling its safety function. Specifically, design features of the CST and the elevation of  
    determining the ABFPs could start with the pumps required minimum flow being
the return line relative to the leak location provided assurance that, in the event the CST  
    achieved through the internal thrust balance lines while the minimum flow lines were
return line leak increased significantly, the CST water volume would have been  
    isolated. In addition, the inspectors interviewed plant staff, and reviewed issues entered
maintained above TS minimum required water level and able to supply the required  
    into the corrective action program to determine whether Entergy had been effective in
water to the auxiliary feedwater system.  
    identifying and resolving problems associated with the temporary modification. The
    documents reviewed are listed in the Attachment.
1R18 Plant Modifications (71111.18 - 2 samples)  
   b. Findings
    No findings of significance were identified.
.1  
                                                                                          Enclosure
Temporary Modifications
 
a.  
Inspection Scope  
The inspectors reviewed one temporary plant modification package for securing  
minimum flow lines on the motor driven auxiliary boiler feedwater pumps (ABFPs) and  
controlling the operation on the ABFPs through a temporary operating procedure during  
repairs of the CST return piping. The inspectors verified the design bases, licensing  
bases, and performance capability of the system was not degraded by the temporary  
modification. The inspectors review included Entergys engineering evaluation for  
determining the ABFPs could start with the pumps required minimum flow being  
achieved through the internal thrust balance lines while the minimum flow lines were  
isolated. In addition, the inspectors interviewed plant staff, and reviewed issues entered  
into the corrective action program to determine whether Entergy had been effective in  
identifying and resolving problems associated with the temporary modification. The  
documents reviewed are listed in the Attachment.  
   b.  
Findings  
No findings of significance were identified.  


                                                21
21  
.2   Permanent Modifications
Enclosure 
  a. Inspection Scope
.2  
    The inspectors reviewed modification documents associated with the installation of an
Permanent Modifications
    additional nitrogen backup power supply for the 21- 24 steam generator atmospheric
   
    dump valves. The inspector verified that the modification was reviewed adequately to
a.  
    verify the modification conformed to design criteria and did not interfere or invalidate
Inspection Scope  
    previous design assumptions or functions. The documents reviewed are listed in the
    Attachment.
The inspectors reviewed modification documents associated with the installation of an  
   b. Findings
additional nitrogen backup power supply for the 21- 24 steam generator atmospheric  
    No findings of significance were identified.
dump valves. The inspector verified that the modification was reviewed adequately to  
1R19 Post-Maintenance Testing (71111.19 - 6 samples)
verify the modification conformed to design criteria and did not interfere or invalidate  
   a. Inspection Scope
previous design assumptions or functions. The documents reviewed are listed in the  
    The inspectors reviewed post-maintenance test procedures and associated testing
Attachment.  
    activities for selected risk-significant mitigating systems, and assessed whether the
    effect of maintenance on plant systems was adequately addressed by control room and
   b.  
    engineering personnel. The inspectors verified that: test acceptance criteria were clear,
Findings  
    the test demonstrated operational readiness and were consistent with design basis
    documentation; test instrumentation had current calibrations, and appropriate range and
    accuracy for the application; and the tests were performed as written, with applicable
No findings of significance were identified.  
    prerequisites satisfied. Upon completion of the tests, the inspectors verified that
    equipment was returned to the proper alignment necessary to perform its safety function.
1R19 Post-Maintenance Testing (71111.19 - 6 samples)  
    Post-maintenance testing was evaluated for conformance with the requirements of 10
    CFR 50, Appendix B, Criterion XI, Test Control. The documents reviewed are listed in
   a.  
    the Attachment. The following post-maintenance activities were reviewed and
Inspection Scope  
    represented six inspection samples:
    *   Replacement of SG 23 pressure indicator PI-1355;
    *   22 component cooling water heat exchanger following maintenance;
The inspectors reviewed post-maintenance test procedures and associated testing  
    *   21 charging pump following recirculation valve maintenance;
activities for selected risk-significant mitigating systems, and assessed whether the  
    *   Condensate storage tank return line following pipe section replacement;
effect of maintenance on plant systems was adequately addressed by control room and  
    *   Emergency diesel generator air compressor following quarterly maintenance; and
engineering personnel. The inspectors verified that: test acceptance criteria were clear,  
    *   23 emergency diesel generator following quarterly engine maintenance.
the test demonstrated operational readiness and were consistent with design basis  
   b. Findings
documentation; test instrumentation had current calibrations, and appropriate range and  
    No findings of significance were identified.
accuracy for the application; and the tests were performed as written, with applicable  
1R22 Surveillance Testing (71111.22 - 6 samples)
prerequisites satisfied. Upon completion of the tests, the inspectors verified that  
   a. Inspection Scope
equipment was returned to the proper alignment necessary to perform its safety function.
    The inspectors observed performance of portions of surveillance tests and/or reviewed
Post-maintenance testing was evaluated for conformance with the requirements of 10  
    test data for selected risk-significant SSCs to assess whether they satisfied Technical
CFR 50, Appendix B, Criterion XI, Test Control. The documents reviewed are listed in  
    Specifications, UFSAR, Technical Requirements Manual, and Entergy procedure
the Attachment. The following post-maintenance activities were reviewed and  
                                                                                      Enclosure
represented six inspection samples:  
*  
Replacement of SG 23 pressure indicator PI-1355;  
*  
22 component cooling water heat exchanger following maintenance;  
*  
21 charging pump following recirculation valve maintenance;  
*  
Condensate storage tank return line following pipe section replacement;  
*  
Emergency diesel generator air compressor following quarterly maintenance; and  
*  
23 emergency diesel generator following quarterly engine maintenance.  
   b.  
Findings  
No findings of significance were identified.  
1R22 Surveillance Testing (71111.22 - 6 samples)  
   a.  
Inspection Scope  
The inspectors observed performance of portions of surveillance tests and/or reviewed  
test data for selected risk-significant SSCs to assess whether they satisfied Technical  
Specifications, UFSAR, Technical Requirements Manual, and Entergy procedure  


                                            22
22  
  requirements. The inspectors verified that: test acceptance criteria were identified,
Enclosure 
  demonstrated operational readiness, and were consistent with design basis
requirements. The inspectors verified that: test acceptance criteria were identified,  
  documentation; test instrumentation had accurate calibration, and appropriate range and
demonstrated operational readiness, and were consistent with design basis  
  accuracy for the application; and tests were performed as written, with applicable
documentation; test instrumentation had accurate calibration, and appropriate range and  
  prerequisites satisfied. Following the tests, the inspectors verified that the equipment
accuracy for the application; and tests were performed as written, with applicable  
  was capable of performing the required safety functions. The inspectors evaluated the
prerequisites satisfied. Following the tests, the inspectors verified that the equipment  
  surveillance tests against the requirements in Technical Specifications. The documents
was capable of performing the required safety functions. The inspectors evaluated the  
  reviewed during this inspection are listed in the Attachment. The following surveillance
surveillance tests against the requirements in Technical Specifications. The documents  
  tests were reviewed and represented six inspection samples:
reviewed during this inspection are listed in the Attachment. The following surveillance  
  *   2-PT-Q031A, 21 Auxiliary Component Cooling Pump In-Service Test;
tests were reviewed and represented six inspection samples:  
  *   2-PT-Q054, Pressurizer Level Bistables;
  *   2-PT-Q013 DS027, IST Valve Test of 888A (Safety Injection Pump Suction from
*  
        Residual Heat Removal heat Exchanger);
2-PT-Q031A, 21 Auxiliary Component Cooling Pump In-Service Test;  
  *   2-PT-2M4, Safety Injection System Train A Actuation Logic and Master Relay Test;
*  
  *   2-PT-Q030C, 23 Component Cooling Water Pump; and
2-PT-Q054, Pressurizer Level Bistables;  
  *   0-SOP-LEAKRATE-001, RCS Leakrate Surveillance, Evaluation, and Leak
*  
        Identification.
2-PT-Q013 DS027, IST Valve Test of 888A (Safety Injection Pump Suction from  
b. Findings
Residual Heat Removal heat Exchanger);  
    Introduction. The inspectors identified a NCV of very low safety significance (Green)
*  
    related to 10 CFR 50.55a, Codes and standards, because Entergys procedure 2-PT-
2-PT-2M4, Safety Injection System Train A Actuation Logic and Master Relay Test;  
    Q031A did not contain appropriate acceptance criteria for determining that safety-
*  
    related check valves performed their safety function when required in accordance with
2-PT-Q030C, 23 Component Cooling Water Pump; and  
    the American Society of Mechanical Engineers (ASME) OM Code.
*  
    Description. Entergy procedure 2-PT-Q031A, 21 Auxiliary Component Cooling Pump
0-SOP-LEAKRATE-001, RCS Leakrate Surveillance, Evaluation, and Leak  
    (ACCP), is an In-Service Test (IST) procedure that demonstrates the operability of the
Identification.  
    21 ACCP, the pump bypass line check valve (755), the 21 ACCP discharge check valve
    (755B), and the 22 ACCP discharge check valve (755A) in accordance with Technical
  b.  
    Specification (TS) 5.5.6, Inservice Testing Program.
Findings  
    The test established a single acceptance criterion to determine if the discharge check
    valve on the 22 ACCP train shuts when the parallel trains 21 ACCP is providing design
Introduction. The inspectors identified a NCV of very low safety significance (Green)  
    flow. The acceptance criterion was that no reverse rotation is observed on the 22
related to 10 CFR 50.55a, Codes and standards, because Entergys procedure 2-PT-
    ACCP. Although NUREG-1482, Guidelines for Inservice Testing at Nuclear Power
Q031A did not contain appropriate acceptance criteria for determining that safety-
    Plants identifies the methodology of using reverse pump rotation as an acceptable
related check valves performed their safety function when required in accordance with  
    means of testing, Entergys site-specific experience in 2005 demonstrated this particular
the American Society of Mechanical Engineers (ASME) OM Code.  
    method was not effective to maintain the ACCP discharge check valve safety function.
    Specifically, when 2-PT-Q031A was performed on January 19, 2005, the 21 ACCP
Description. Entergy procedure 2-PT-Q031A, 21 Auxiliary Component Cooling Pump  
    failed the performance test because check valve 755A was determined to be in the
(ACCP), is an In-Service Test (IST) procedure that demonstrates the operability of the  
    open position. However, the 22 ACCP did not rotate in the reverse direction. Following
21 ACCP, the pump bypass line check valve (755), the 21 ACCP discharge check valve  
    disassembly of valve 755A, engineers determined the valve remained in the open
(755B), and the 22 ACCP discharge check valve (755A) in accordance with Technical  
    position because of excessive clearances between the hinge pin and hinge pin
Specification (TS) 5.5.6, Inservice Testing Program.  
    bushings. Entergy personnel determined the check valve was likely in this condition
    following maintenance on the valve in late 2004. CR-IP2-2005-0252 was written to
The test established a single acceptance criterion to determine if the discharge check  
    document and evaluate the issue. The issue was previously documented in LER
valve on the 22 ACCP train shuts when the parallel trains 21 ACCP is providing design  
    05000247/2005001-00 and NRC NCV 50-247/2005003-01. At that time, Entergy
flow. The acceptance criterion was that no reverse rotation is observed on the 22  
    personnel concluded the test criteria established in 2-PT-Q031A was acceptable but
ACCP. Although NUREG-1482, Guidelines for Inservice Testing at Nuclear Power  
    that post-maintenance tests on the check valve should include amplifying comments
Plants identifies the methodology of using reverse pump rotation as an acceptable  
                                                                                      Enclosure
means of testing, Entergys site-specific experience in 2005 demonstrated this particular  
method was not effective to maintain the ACCP discharge check valve safety function.
Specifically, when 2-PT-Q031A was performed on January 19, 2005, the 21 ACCP  
failed the performance test because check valve 755A was determined to be in the  
open position. However, the 22 ACCP did not rotate in the reverse direction. Following  
disassembly of valve 755A, engineers determined the valve remained in the open  
position because of excessive clearances between the hinge pin and hinge pin  
bushings. Entergy personnel determined the check valve was likely in this condition  
following maintenance on the valve in late 2004. CR-IP2-2005-0252 was written to  
document and evaluate the issue. The issue was previously documented in LER  
05000247/2005001-00 and NRC NCV 50-247/2005003-01. At that time, Entergy  
personnel concluded the test criteria established in 2-PT-Q031A was acceptable but  
that post-maintenance tests on the check valve should include amplifying comments  


                                          23
23  
directing the performance of the IST following maintenance. Entergy personnel
Enclosure 
concluded that the IST was adequate because the low pump head that caused the
directing the performance of the IST following maintenance. Entergy personnel  
pump performance test to fail led to troubleshooting that identified that check valve
concluded that the IST was adequate because the low pump head that caused the  
755A was stuck open.
pump performance test to fail led to troubleshooting that identified that check valve  
755A was stuck open.  
The inspectors determined that the criterion for determining operability of 755A in test 2-
The inspectors determined that the criterion for determining operability of 755A in test 2-
PT-Q013A was inadequate because the criterion in the procedure previously failed to
PT-Q013A was inadequate because the criterion in the procedure previously failed to  
identify that 755A remained in the open position in January 2005 and 2-PT-Q013A does
identify that 755A remained in the open position in January 2005 and 2-PT-Q013A does  
not identify any other criteria, including using pump head, to determine operability of
not identify any other criteria, including using pump head, to determine operability of  
755A. Additionally, the inspectors determined the test criterion for check valve 755A
755A. Additionally, the inspectors determined the test criterion for check valve 755A  
and 755B were not consistent with the following ASME Code requirements:
and 755B were not consistent with the following ASME Code requirements:  
*   The ASME OM Code 2001 Subsection ISTA-3160 states that procedures shall
    contain the Owner-specified reference values and acceptance criteria;
*  
*   The ASME OM Code 2001 Subsection ISTC-1400 (c) states it is the Owners
The ASME OM Code 2001 Subsection ISTA-3160 states that procedures shall  
    responsibility to ensure that the application, method, and capability of each
contain the Owner-specified reference values and acceptance criteria;  
    nonintrusive technique is qualified; and
*  
*   The ASME OM Code 2001 Subsection ISTC-3530 states obturator movement
The ASME OM Code 2001 Subsection ISTC-1400 (c) states it is the Owners  
    shall be determined by exercising the valve while observing an appropriate
responsibility to ensure that the application, method, and capability of each  
    indicator.
nonintrusive technique is qualified; and  
Analysis. The inspectors determined that the performance deficiency was more than
*  
minor because it was associated with the procedure quality attribute of the Mitigating
The ASME OM Code 2001 Subsection ISTC-3530 states obturator movement  
System cornerstone and adversely affected the cornerstone objective to ensure the
shall be determined by exercising the valve while observing an appropriate  
reliability of systems that respond to initiating events to prevent undesirable
indicator.  
consequences. Specifically, the test criterion used in procedure 2-PT-Q013A did not
ensure that valve 755A reliably performed its safety function when tested as
Analysis. The inspectors determined that the performance deficiency was more than  
demonstrated by testing performed in January 2005. The inspectors determined that
minor because it was associated with the procedure quality attribute of the Mitigating  
the performance deficiency was of very low safety significance (Green) using IMC 0609,
System cornerstone and adversely affected the cornerstone objective to ensure the  
Attachment 4, Phase 1 - Initial Screening and Characterization of Findings.
reliability of systems that respond to initiating events to prevent undesirable  
Specifically, the inspectors determined that this finding was of very low safety
consequences. Specifically, the test criterion used in procedure 2-PT-Q013A did not  
significance because the finding did not result in a loss of safety function and did not
ensure that valve 755A reliably performed its safety function when tested as  
screen as potentially risk-significant due to external events initiating events.
demonstrated by testing performed in January 2005. The inspectors determined that  
The inspectors determined the finding had a cross-cutting aspect related to effective
the performance deficiency was of very low safety significance (Green) using IMC 0609,  
corrective actions in the corrective action program component of the problem
Attachment 4, Phase 1 - Initial Screening and Characterization of Findings.
identification and resolution area. Specifically, Entergy did not implement effective
Specifically, the inspectors determined that this finding was of very low safety  
corrective actions to resolve the testing inadequacy since 2005 during subsequent
significance because the finding did not result in a loss of safety function and did not  
quarterly testing. Additionally, the issue was considered to be indicative of current
screen as potentially risk-significant due to external events initiating events.  
performance because personnel when initially responding to inspector questions
concluded the acceptance criteria were adequate. (P.1(d) per IMC 0305)
The inspectors determined the finding had a cross-cutting aspect related to effective  
Enforcement. 10 CFR 50.55a, Codes and standards, states that pumps and valves
corrective actions in the corrective action program component of the problem  
which are classified as ASME code Class 1, Class 2, and Class 3 must meet the
identification and resolution area. Specifically, Entergy did not implement effective  
inservice test requirements set forth in the ASME OM Code (2001 edition for Indian
corrective actions to resolve the testing inadequacy since 2005 during subsequent  
Point Unit 2). Furthermore, inservice tests to verify operational readiness of pumps and
quarterly testing. Additionally, the issue was considered to be indicative of current  
valves, whose function is required for safety must comply with the requirements of the
performance because personnel when initially responding to inspector questions  
ASME OM Code. The ASME OM Code 2001 Subsection ISTC-1400 (c) states it is the
concluded the acceptance criteria were adequate. (P.1(d) per IMC 0305)  
Owners responsibility to ensure that the application, method, and capability of each
nonintrusive technique is qualified. In addition, the ASME OM Code 2001 Subsection
Enforcement. 10 CFR 50.55a, Codes and standards, states that pumps and valves  
ISTC-3530 states obturator movement shall be determined by exercising the valve
which are classified as ASME code Class 1, Class 2, and Class 3 must meet the  
                                                                                  Enclosure
inservice test requirements set forth in the ASME OM Code (2001 edition for Indian  
Point Unit 2). Furthermore, inservice tests to verify operational readiness of pumps and  
valves, whose function is required for safety must comply with the requirements of the  
ASME OM Code. The ASME OM Code 2001 Subsection ISTC-1400 (c) states it is the  
Owners responsibility to ensure that the application, method, and capability of each  
nonintrusive technique is qualified. In addition, the ASME OM Code 2001 Subsection  
ISTC-3530 states obturator movement shall be determined by exercising the valve  


                                                24
24  
      while observing an appropriate indicator. Contrary to the above, from February 2005
Enclosure 
      until February 2009, Entergy procedure 2-PT-Q031A, did not include appropriate
while observing an appropriate indicator. Contrary to the above, from February 2005  
      acceptance criteria for demonstrating operability of valve 755A. Specifically, the test did
until February 2009, Entergy procedure 2-PT-Q031A, did not include appropriate  
      not utilize a qualified technique for testing the check-valve and did not verify check valve
acceptance criteria for demonstrating operability of valve 755A. Specifically, the test did  
      movement by observing an appropriate indicator. Because ACCP performance tests
not utilize a qualified technique for testing the check-valve and did not verify check valve  
      since 2004 demonstrated satisfactory performance of the ACCPs at design flows, no
movement by observing an appropriate indicator. Because ACCP performance tests  
      actual impact to the operability of the ACCPs was evident. Because this violation was
since 2004 demonstrated satisfactory performance of the ACCPs at design flows, no  
      of very low safety significance and it was entered into Entergys corrective action
actual impact to the operability of the ACCPs was evident. Because this violation was  
      program (IP2-2009-1312), this violation is being treated as an NCV, consistent with the
of very low safety significance and it was entered into Entergys corrective action  
      NRC Enforcement Policy. NCV 2009002-06, Inadequate Test Acceptance Criteria
program (IP2-2009-1312), this violation is being treated as an NCV, consistent with the  
      for Auxiliary Component Cooling Check Valves.
NRC Enforcement Policy. NCV 2009002-06, Inadequate Test Acceptance Criteria  
    Cornerstone: Emergency Preparedness (EP)
for Auxiliary Component Cooling Check Valves.  
1EP6 Drill Evaluation (71114.06 - 1 sample)
  a. Inspection Scope
Cornerstone: Emergency Preparedness (EP)  
    The inspectors evaluated an emergency classification conducted on February 23, 2009,
    during a licensed-operator requalification simulator training evaluation. The inspectors
1EP6 Drill Evaluation (71114.06 - 1 sample)  
    observed an operating crew in the simulator respond to various, simulated initiating
   
    events that ultimately resulted in the simulated implementation of the emergency plan.
  a.  
    In particular, the inspectors verified the adequacy and accuracy of the simulated
Inspection Scope  
    emergency classification of a Site Area Emergency. While other simulated
    classifications were made, the inspectors verified that the initial classification was
The inspectors evaluated an emergency classification conducted on February 23, 2009,  
    appropriately credited as an opportunity toward NRC performance indicator data. The
during a licensed-operator requalification simulator training evaluation. The inspectors  
    inspectors observed the management evaluator and training critique following
observed an operating crew in the simulator respond to various, simulated initiating  
    termination of the scenarios, and verified that significant performance deficiencies were
events that ultimately resulted in the simulated implementation of the emergency plan.
    appropriately identified and addressed within the critique and the corrective action
In particular, the inspectors verified the adequacy and accuracy of the simulated  
    program. Also, the inspectors reviewed the summary performance report for the
emergency classification of a Site Area Emergency. While other simulated  
    evaluation and verified that appropriate attributes of drill performance including
classifications were made, the inspectors verified that the initial classification was  
    deficiencies were captured. This evaluation constituted one inspection sample.
appropriately credited as an opportunity toward NRC performance indicator data. The  
  b.  Findings
inspectors observed the management evaluator and training critique following  
    No findings of significance were identified.
termination of the scenarios, and verified that significant performance deficiencies were  
2.   RADIATION SAFETY
appropriately identified and addressed within the critique and the corrective action  
    Cornerstone: Occupational Radiation Safety (OS)
program. Also, the inspectors reviewed the summary performance report for the  
2OS1 Access Control to Radiologically Significant Areas (71121.01 - 16 samples)
evaluation and verified that appropriate attributes of drill performance including  
  a. Inspection Scope
deficiencies were captured. This evaluation constituted one inspection sample.  
    From March 23 through March 27, 2009, the inspectors conducted the following
   
    activities to verify that Entergy was properly implementing physical, engineering, and
  b.  
    administrative controls for access to high radiation areas, and other radiologically
Findings
    controlled areas, and that workers were adhering to these controls when working in
    these areas. Implementation of the access control program was reviewed against the
   
                                                                                        Enclosure
No findings of significance were identified.  
2.  
RADIATION SAFETY  
Cornerstone: Occupational Radiation Safety (OS)  
2OS1 Access Control to Radiologically Significant Areas (71121.01 - 16 samples)  
   
  a.  
Inspection Scope  
From March 23 through March 27, 2009, the inspectors conducted the following  
activities to verify that Entergy was properly implementing physical, engineering, and  
administrative controls for access to high radiation areas, and other radiologically  
controlled areas, and that workers were adhering to these controls when working in  
these areas. Implementation of the access control program was reviewed against the  


                                            25
25  
criteria contained in 10 CFR 20, site technical specifications, and Entergys procedures
Enclosure 
required by the Technical Specifications as criteria for determining compliance.
criteria contained in 10 CFR 20, site technical specifications, and Entergys procedures  
This inspection activity represents completion of sixteen (16) samples relative to this
required by the Technical Specifications as criteria for determining compliance.  
inspection area. The inspector performed independent radiation dose rate
This inspection activity represents completion of sixteen (16) samples relative to this  
measurements and reviewed the following items:
inspection area. The inspector performed independent radiation dose rate  
Plant Walk Downs and Radiological Work Permit Reviews
measurements and reviewed the following items:  
(1)     Exposure significant work areas were identified by inspectors for review within
        radiation areas, high radiation areas, and airborne areas in the plant. Associated
Plant Walk Downs and Radiological Work Permit Reviews  
        licensee controls and surveys were review for adequacy. Work reviewed
        included: Refuel Floor Split Pin and Reactor Head Inspections, Refuel Floor
(1)  
        Lower Internals Removal and Installation, Refuel Floor and Fuel Support Building
Exposure significant work areas were identified by inspectors for review within  
        Fuel Transport Equipment Repairs requiring an underwater diver, Reactor
radiation areas, high radiation areas, and airborne areas in the plant. Associated  
        Coolant Pump work including RCP #31 Impeller replacement, Containment valve
licensee controls and surveys were review for adequacy. Work reviewed  
        work including Pressurizer Safety Valves, Various Containment and Auxiliary
included: Refuel Floor Split Pin and Reactor Head Inspections, Refuel Floor  
        Building activities.
Lower Internals Removal and Installation, Refuel Floor and Fuel Support Building  
(2)     With a survey instrument and assistance from a health physics technician,
Fuel Transport Equipment Repairs requiring an underwater diver, Reactor  
        inspectors walked down the above mentioned areas to determine: whether the
Coolant Pump work including RCP #31 Impeller replacement, Containment valve  
        radiation work permits (RWPs), procedures and engineering controls were in
work including Pressurizer Safety Valves, Various Containment and Auxiliary  
        place and whether surveys and postings were adequate.
Building activities.  
(3)     The inspectors reviewed RWPs that provide access to exposure significant areas
        of the plant including high radiation areas. Specified electronic personal
(2)  
        dosimeter alarm set points were reviewed with respect to current radiological
With a survey instrument and assistance from a health physics technician,  
        condition applicability and workers were queried to verify their understanding of
inspectors walked down the above mentioned areas to determine: whether the  
        plant procedures governing alarm response and knowledge of radiological
radiation work permits (RWPs), procedures and engineering controls were in  
        conditions in their work area.
place and whether surveys and postings were adequate.  
(4)     There were no radiation work permits for airborne radioactivity areas with the
        potential for individual worker internal exposures of >50 mrem CEDE.
(3)  
(5)     There were no internal dose assessments that resulted in actual internal
The inspectors reviewed RWPs that provide access to exposure significant areas  
        exposures greater than 50 mrem CEDE. Internal assessments were reviewed to
of the plant including high radiation areas. Specified electronic personal  
        determine adequacy and assurance that they were not in fact equal to or greater
dosimeter alarm set points were reviewed with respect to current radiological  
        than 50 mrem CEDE.
condition applicability and workers were queried to verify their understanding of  
Problem Identification and Resolution
plant procedures governing alarm response and knowledge of radiological  
(6)     Access controls related condition reports were reviewed since the last inspection
conditions in their work area.  
        in this area. Staff members were interviewed and documents reviewed to
        determine that follow-up activities are being conducted in an effective and timely
(4)  
        manner, commensurate with their safety and risk.
There were no radiation work permits for airborne radioactivity areas with the  
(7)     For repetitive deficiencies or significant individual deficiencies in problem
potential for individual worker internal exposures of >50 mrem CEDE.  
        identification and resolution, the inspectors determined if the licensees
        assessment activities were also identifying and addressing these deficiencies.
(5)  
(8)     A review of events revealed no performance indicator occurrences that involved
There were no internal dose assessments that resulted in actual internal  
        dose rates greater than 25 Rem/hour at 30 cm, dose rates greater than
exposures greater than 50 mrem CEDE. Internal assessments were reviewed to  
                                                                                    Enclosure
determine adequacy and assurance that they were not in fact equal to or greater  
than 50 mrem CEDE.  
Problem Identification and Resolution  
(6)  
Access controls related condition reports were reviewed since the last inspection  
in this area. Staff members were interviewed and documents reviewed to  
determine that follow-up activities are being conducted in an effective and timely  
manner, commensurate with their safety and risk.  
(7)  
For repetitive deficiencies or significant individual deficiencies in problem  
identification and resolution, the inspectors determined if the licensees  
assessment activities were also identifying and addressing these deficiencies.  
(8)  
A review of events revealed no performance indicator occurrences that involved  
dose rates greater than 25 Rem/hour at 30 cm, dose rates greater than  


                                        26
26  
      500 Rem/hour at 1 meter, or unintended exposures greater than 100 mrem
Enclosure 
      TEDE (or greater than 5 Rem SDE or greater than 1.5 Rem LDE)
500 Rem/hour at 1 meter, or unintended exposures greater than 100 mrem  
Job-in-Progress Reviews
TEDE (or greater than 5 Rem SDE or greater than 1.5 Rem LDE)  
(9)   The inspectors observed aspects of various on-going activities to confirm that
      radiological controls, such as required surveys, area postings, job coverage, and
Job-in-Progress Reviews  
      job site preparations were conducted. The inspectors verified that personnel
      dosimetry was properly worn and that workers were knowledgeable of work area
(9)  
      conditions. The inspectors attended pre-planning meetings for work described
The inspectors observed aspects of various on-going activities to confirm that  
      earlier in the report.
radiological controls, such as required surveys, area postings, job coverage, and  
(10)   Underwater diving activities associated with repairs to the fuel transport system
job site preparations were conducted. The inspectors verified that personnel  
      were reviewed for adequacy. Dosimetry requirements, bioassay requirements,
dosimetry was properly worn and that workers were knowledgeable of work area  
      and controls were reviewed.
conditions. The inspectors attended pre-planning meetings for work described  
High Risk Significant, High Dose Rate High Radiation Areas (HRA) and Very HRA
earlier in the report.  
Controls
(11)   Keys to locked and very HRA were reviewed for their controls and proper
(10)  
      inventory. Accessible locked HRA were verified to be properly secured and
Underwater diving activities associated with repairs to the fuel transport system  
      posted during plant tours.
were reviewed for adequacy. Dosimetry requirements, bioassay requirements,  
(12)   The inspectors discussed with Radiation Protection supervision the adequacy of
and controls were reviewed.  
      high dose rate HRA controls and procedures and verified that no programmatic
      or procedural changes have occurred that reduce the effectiveness and level of
High Risk Significant, High Dose Rate High Radiation Areas (HRA) and Very HRA  
      worker protection.
Controls  
Radiation Worker Performance
(13)   During observation of the work activities listed above, radiation worker
(11)  
      performance was evaluated with respect to the specific radiation protection work
Keys to locked and very HRA were reviewed for their controls and proper  
      requirements and their knowledge of the radiological conditions in their work
inventory. Accessible locked HRA were verified to be properly secured and  
      areas.
posted during plant tours.  
(14)   The inspectors reviewed condition reports, related to radiation worker
      performance to determine if an observable pattern traceable to a similar cause
(12)  
      was evident.
The inspectors discussed with Radiation Protection supervision the adequacy of  
Radiation Protection Technician Proficiency
high dose rate HRA controls and procedures and verified that no programmatic  
(15)   During observation of the work activities listed above, radiation protection
or procedural changes have occurred that reduce the effectiveness and level of  
      technician work performance was evaluated with respect to their knowledge of
worker protection.  
      the radiological conditions, the specific radiation protection work requirements
      and radiation protection procedures.
Radiation Worker Performance  
(16)   The inspectors reviewed condition reports, related to radiation worker
      performance to determine if an observable pattern traceable to a similar cause
(13)  
      was evident.
During observation of the work activities listed above, radiation worker  
                                                                                  Enclosure
performance was evaluated with respect to the specific radiation protection work  
requirements and their knowledge of the radiological conditions in their work  
areas.  
(14)  
The inspectors reviewed condition reports, related to radiation worker  
performance to determine if an observable pattern traceable to a similar cause  
was evident.  
Radiation Protection Technician Proficiency  
(15)  
During observation of the work activities listed above, radiation protection  
technician work performance was evaluated with respect to their knowledge of  
the radiological conditions, the specific radiation protection work requirements  
and radiation protection procedures.  
(16)  
The inspectors reviewed condition reports, related to radiation worker  
performance to determine if an observable pattern traceable to a similar cause  
was evident.  


                                            27
27  
b. Findings
Enclosure 
  Introduction. The inspectors identified a NCV of very low safety significance (Green)
  b.  
  related to Technical Specification 5.4.1.a, Procedures, because Entergy personnel did
Findings  
  not generate condition reports or investigation paperwork for multiple high dose-rate
  alarms as required by station procedures. Specifically, personnel did not generate the
Introduction. The inspectors identified a NCV of very low safety significance (Green)  
  required condition reports and adequately document the investigations for six instances
related to Technical Specification 5.4.1.a, Procedures, because Entergy personnel did  
  of unplanned or un-briefed electronic dosimeter alarms received by individuals in the
not generate condition reports or investigation paperwork for multiple high dose-rate  
  Unit 2 radiologically controlled area (RCA) that occurred between January 2009 and
alarms as required by station procedures. Specifically, personnel did not generate the  
  March 2009.
required condition reports and adequately document the investigations for six instances  
  Description. During the period January 2009 through March 2009, six instances of
of unplanned or un-briefed electronic dosimeter alarms received by individuals in the  
  electronic dosimeter dose rate alarms were recorded by the access control system for
Unit 2 radiologically controlled area (RCA) that occurred between January 2009 and  
  Unit 2 personnel in the RCA (Unit 3 had 15 instances). During this period, Entergy
March 2009.  
  personnel inconsistently utilized an informal process of reviewing the alarms without a
  full investigation or approval process. Moreover, in one of the six instances at Unit 2,
Description. During the period January 2009 through March 2009, six instances of  
  the inspectors identified that no investigation or follow-up had occurred. In some cases,
electronic dosimeter dose rate alarms were recorded by the access control system for  
  the occurrences were over two months old, which the inspectors noted would have
Unit 2 personnel in the RCA (Unit 3 had 15 instances). During this period, Entergy  
  made resultant investigations more challenging to perform. In other cases, the alarms
personnel inconsistently utilized an informal process of reviewing the alarms without a  
  were not identified until the worker attempted to re-enter the RCA and the access control
full investigation or approval process. Moreover, in one of the six instances at Unit 2,  
  system required manual override to un-lock the occurrence to allow entry into the RCA.
the inspectors identified that no investigation or follow-up had occurred. In some cases,  
  The inspectors noted that the controlling Entergy procedure for this activity, EN-RP-203,
the occurrences were over two months old, which the inspectors noted would have  
  Dose Assessment, specifies that for a dose-rate alarm that is unanticipated or un-
made resultant investigations more challenging to perform. In other cases, the alarms  
  briefed, several actions are required, one of which is to initiate a condition report,
were not identified until the worker attempted to re-enter the RCA and the access control  
  another is to document the investigation using an attachment in the procedure. Contrary
system required manual override to un-lock the occurrence to allow entry into the RCA.
  to EN-RP-203, for these 21 instances, no condition reports or attachments were
The inspectors noted that the controlling Entergy procedure for this activity, EN-RP-203,  
  generated with a detailed investigation prior to the workers re-entering the radiologically
Dose Assessment, specifies that for a dose-rate alarm that is unanticipated or un-
  controlled area. The highest exposure received by these workers during their entry, as
briefed, several actions are required, one of which is to initiate a condition report,  
  indicated by their electronic dosimeter and logged by the access control system, was 33
another is to document the investigation using an attachment in the procedure. Contrary  
  mRem, while most dosimeters indicated less than 1 mRem for the entry.
to EN-RP-203, for these 21 instances, no condition reports or attachments were  
  Analysis. The inspectors determined that the failure to generate a condition report, as
generated with a detailed investigation prior to the workers re-entering the radiologically  
  well as the failure to adequately investigate six unplanned or un-briefed electronic
controlled area. The highest exposure received by these workers during their entry, as  
  dosimeter alarms prior to re-entry into the Unit 2 RCA, as required by station procedure
indicated by their electronic dosimeter and logged by the access control system, was 33  
  was a performance deficiency. This performance deficiency was within Entergy
mRem, while most dosimeters indicated less than 1 mRem for the entry.  
  personnels ability to foresee and correct, and should have been prevented. This issue
  was not subject to traditional enforcement, in that it did not have actual safety
Analysis. The inspectors determined that the failure to generate a condition report, as  
  consequence, it was not an issue that had the potential to impact NRCs ability to
well as the failure to adequately investigate six unplanned or un-briefed electronic  
  perform its regulatory function, and there were no willful aspects.
dosimeter alarms prior to re-entry into the Unit 2 RCA, as required by station procedure  
  The finding is more than minor because it is associated with the Occupational Radiation
was a performance deficiency. This performance deficiency was within Entergy  
  Safety cornerstone attribute of programs and process, and adversely affected its
personnels ability to foresee and correct, and should have been prevented. This issue  
  objective to ensure adequate protection of worker health and safety from exposure to
was not subject to traditional enforcement, in that it did not have actual safety  
  radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and
consequence, it was not an issue that had the potential to impact NRCs ability to  
  implement programs to keep exposures as low as reasonably achievable, because
perform its regulatory function, and there were no willful aspects.  
  multiple examples were identified regarding the failure to satisfy station radiation
  protection procedures. Specifically, in six cases, Entergy did not fully evaluate dose rate
The finding is more than minor because it is associated with the Occupational Radiation  
  alarms received by workers in radiologically controlled areas of the plant. Using the
Safety cornerstone attribute of programs and process, and adversely affected its  
  Occupational Radiation Safety Significance Determination Process, the inspectors
objective to ensure adequate protection of worker health and safety from exposure to  
  determined that the finding was of very low safety significance (Green) because it did not
radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and  
  involve: (1) as low as is reasonably achievable planning and controls, (2) an
implement programs to keep exposures as low as reasonably achievable, because  
                                                                                      Enclosure
multiple examples were identified regarding the failure to satisfy station radiation  
protection procedures. Specifically, in six cases, Entergy did not fully evaluate dose rate  
alarms received by workers in radiologically controlled areas of the plant. Using the  
Occupational Radiation Safety Significance Determination Process, the inspectors  
determined that the finding was of very low safety significance (Green) because it did not  
involve: (1) as low as is reasonably achievable planning and controls, (2) an  


                                                28
28  
    overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to
Enclosure 
    assess dose.
overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to  
    The inspectors determined that the finding had a cross-cutting aspect related to
assess dose.  
    procedural adherence in the Work Practices component of the Human Performance
    area. Specifically, Entergy employees did not follow procedures to generate condition
The inspectors determined that the finding had a cross-cutting aspect related to  
    reports and document investigations when high-dose rate alarms were received by
procedural adherence in the Work Practices component of the Human Performance  
    workers. (H.4 (b) per IMC 0305)
area. Specifically, Entergy employees did not follow procedures to generate condition  
    Enforcement. Technical Specification 5.4.1.a, Procedures, requires that Entergy
reports and document investigations when high-dose rate alarms were received by  
    establish, implement, and maintain procedures specified in Regulatory Guide (RG) 1.33,
workers. (H.4 (b) per IMC 0305)  
    Revision 2, Appendix A., Section 7.e, radiation protection procedures for personnel
    monitoring. Entergy procedure EN-RP-203, Revision 2, Section 5.11, requires that a
Enforcement. Technical Specification 5.4.1.a, Procedures, requires that Entergy  
    condition report be written for each unplanned or un-briefed electronic dosimeter dose-
establish, implement, and maintain procedures specified in Regulatory Guide (RG) 1.33,  
    rate alarm. Contrary to the above, the inspectors identified through a review of
Revision 2, Appendix A., Section 7.e, radiation protection procedures for personnel  
    electronic dosimeter log information from January 2009 through March 2009, six
monitoring. Entergy procedure EN-RP-203, Revision 2, Section 5.11, requires that a  
    instances of unanticipated or un-briefed electronic dosimeter dose-rate alarms when the
condition report be written for each unplanned or un-briefed electronic dosimeter dose-
    procedure was not implemented and condition reports were not generated. Because
rate alarm. Contrary to the above, the inspectors identified through a review of  
    this finding was of very low safety significance and it was entered into the corrective
electronic dosimeter log information from January 2009 through March 2009, six  
    action program as CR-IP3-2009-001253 and CR-IP3-2009-001318, this violation is
instances of unanticipated or un-briefed electronic dosimeter dose-rate alarms when the  
    being treated as an NCV, consistent with the NRC Enforcement Policy. NCV
procedure was not implemented and condition reports were not generated. Because  
    05000247/2009002-07, Failure to Follow Radiation Protection Procedures.
this finding was of very low safety significance and it was entered into the corrective  
2OS2 ALARA Planning and Controls (71121.02 - 12 samples)
action program as CR-IP3-2009-001253 and CR-IP3-2009-001318, this violation is  
  a. Inspection Scope
being treated as an NCV, consistent with the NRC Enforcement Policy. NCV  
    From March 23 through March 27, 2009, the inspectors conducted the following
05000247/2009002-07, Failure to Follow Radiation Protection Procedures.  
    activities to verify that Entergy was properly maintaining individual and collective
    radiation exposures as low as is reasonably achievable (ALARA). Implementation of the
2OS2 ALARA Planning and Controls (71121.02 - 12 samples)  
    ALARA program was reviewed by inspectors against the criteria contained in 10 CFR
   
    20, applicable industry standards, and Entergys procedures.
  a.  
    This inspection activity represents completion of twelve (12) samples relative to this
Inspection Scope  
    inspection area.
    Inspection Planning
From March 23 through March 27, 2009, the inspectors conducted the following  
    (1)     The inspectors reviewed pertinent information regarding cumulative exposure
activities to verify that Entergy was properly maintaining individual and collective  
              history, current exposure trends, and on-going activities to assess current
radiation exposures as low as is reasonably achievable (ALARA). Implementation of the  
              performance and outage exposure challenges. The inspectors determined the
ALARA program was reviewed by inspectors against the criteria contained in 10 CFR  
              sites 3-year rolling collective average exposure.
20, applicable industry standards, and Entergys procedures.  
    (2)     The inspectors reviewed unit 3 outage work related activities occurring during the
              inspection period, the associated ALARA plans, RWPs, ALARA Committee
This inspection activity represents completion of twelve (12) samples relative to this  
              Reviews, exposure estimates, actual exposures and post job reviews. Work
inspection area.  
              reviewed included: Refuel Floor Split Pin and Reactor Head Inspections, Refuel
              Floor Lower Internals Removal and Installation, Refuel Floor and Fuel Support
Inspection Planning  
              Building Fuel Transport Equipment Repairs requiring an underwater diver,
              Reactor Coolant Pump work including RCP #31 Impeller replacement,
(1)  
                                                                                        Enclosure
The inspectors reviewed pertinent information regarding cumulative exposure  
history, current exposure trends, and on-going activities to assess current  
performance and outage exposure challenges. The inspectors determined the  
sites 3-year rolling collective average exposure.  
(2)  
The inspectors reviewed unit 3 outage work related activities occurring during the  
inspection period, the associated ALARA plans, RWPs, ALARA Committee  
Reviews, exposure estimates, actual exposures and post job reviews. Work  
reviewed included: Refuel Floor Split Pin and Reactor Head Inspections, Refuel  
Floor Lower Internals Removal and Installation, Refuel Floor and Fuel Support  
Building Fuel Transport Equipment Repairs requiring an underwater diver,  
Reactor Coolant Pump work including RCP #31 Impeller replacement,  


                                          29
29  
        Containment valve work including Pressurizer Safety Valves, Various
Enclosure 
        Containment and Auxiliary Building activities.
Containment valve work including Pressurizer Safety Valves, Various  
(3)     The inspectors reviewed implementing procedures associated with maintaining
Containment and Auxiliary Building activities.  
        occupational exposures ALARA. This included a review of the processes used to
        estimate and track work activity exposures.
(3)  
Radiological Work Planning
The inspectors reviewed implementing procedures associated with maintaining  
(4)     With respect to the work activities listed above, the inspectors reviewed dose
occupational exposures ALARA. This included a review of the processes used to  
        summary reports, related post-job ALARA reviews, related RWPS, exposure
estimate and track work activity exposures.  
        estimates and actual exposures, and ALARA Committee meeting paperwork.
        Through this review, the inspector determined that dose was appropriately
Radiological Work Planning  
        managed and evaluated by Station Management.
(5)     ALARA work activity evaluations, exposure estimates, and exposure mitigating
(4)  
        requirements were reviewed for work packages previously mentioned. The
With respect to the work activities listed above, the inspectors reviewed dose  
        inspectors determined that Entergy established procedures, engineering and
summary reports, related post-job ALARA reviews, related RWPS, exposure  
        work controls, based on sound radiation protection principles.
estimates and actual exposures, and ALARA Committee meeting paperwork.  
(6)     The inspectors compared the results achieved with the intended dose that was
Through this review, the inspector determined that dose was appropriately  
        established in the planning of the work. The inspectors determined the reasons
managed and evaluated by Station Management.  
        for any inconsistencies between the intended and actual work activity doses and
        station management awareness and involvement.
(5)  
(7)     The inspectors evaluated for adequacy, the interfaces between operations,
ALARA work activity evaluations, exposure estimates, and exposure mitigating  
        radiation protection, maintenance, maintenance planning and others for interface
requirements were reviewed for work packages previously mentioned. The  
        problems or missing program elements.
inspectors determined that Entergy established procedures, engineering and  
Verification of Dose Estimates and Exposure Tracking Systems
work controls, based on sound radiation protection principles.  
(8)     Methods for adjusting exposure estimates, or re-planning work, when
        unexpected changes in scope or emergent work is encountered, was reviewed
(6)  
        by the inspectors for adequacy.
The inspectors compared the results achieved with the intended dose that was  
Job Site Inspections and ALARA Controls
established in the planning of the work. The inspectors determined the reasons  
(9)     The inspectors reviewed work activities that present the highest radiological risk
for any inconsistencies between the intended and actual work activity doses and  
        to workers. The inspectors evaluated Entergys use of engineering controls to
station management awareness and involvement.  
        achieve dose reductions and to verify that procedures and controls are consistent
        with ALARA reviews. Associated ALARA Plans and RWPs were reviewed to
(7)  
        determine if appropriate exposure and contamination controls were being
The inspectors evaluated for adequacy, the interfaces between operations,  
        employed.
radiation protection, maintenance, maintenance planning and others for interface  
Radiation Worker Performance
problems or missing program elements.  
(10)   Through observations and interviews, workers and technicians were found to be
        knowledgeable of the work area radiological conditions and low dose waiting
Verification of Dose Estimates and Exposure Tracking Systems  
        areas.
                                                                                Enclosure
(8)  
Methods for adjusting exposure estimates, or re-planning work, when  
unexpected changes in scope or emergent work is encountered, was reviewed  
by the inspectors for adequacy.  
Job Site Inspections and ALARA Controls  
(9)  
The inspectors reviewed work activities that present the highest radiological risk  
to workers. The inspectors evaluated Entergys use of engineering controls to  
achieve dose reductions and to verify that procedures and controls are consistent  
with ALARA reviews. Associated ALARA Plans and RWPs were reviewed to  
determine if appropriate exposure and contamination controls were being  
employed.  
Radiation Worker Performance  
(10)  
Through observations and interviews, workers and technicians were found to be  
knowledgeable of the work area radiological conditions and low dose waiting  
areas.  


                                              30
30  
    Declared Pregnant Workers
Enclosure 
    (11)     The inspectors reviewed information associated with declared pregnant workers
Declared Pregnant Workers  
              during the assessment period and whether appropriate monitoring and controls
              were being utilized to ensure compliance with 10CFR Part 20.
(11)  
    Problem Identification and Resolution
The inspectors reviewed information associated with declared pregnant workers  
    (12)     The inspectors reviewed elements of the Entergys corrective action program
during the assessment period and whether appropriate monitoring and controls  
              related to implementing radiological controls to determine if problems are being
were being utilized to ensure compliance with 10CFR Part 20.  
              entered into the program for timely resolution.
  b.  Findings
Problem Identification and Resolution  
    No findings of significance were identified.
4.   OTHER ACTIVITIES [OA]
(12)  
4OA1 Performance Indicator Verification (71151 - 3 samples)
The inspectors reviewed elements of the Entergys corrective action program  
  a. Inspection Scope
related to implementing radiological controls to determine if problems are being  
    The inspectors reviewed performance indicator data for the cornerstones listed below
entered into the program for timely resolution.  
    and used Nuclear Energy Institute 99-02, Regulatory Assessment Performance
   
    Indicator Guideline, Revision 5, to verify individual performance indicator accuracy and
  b.  
    completeness. The documents reviewed during this inspection are listed in the
Findings
    Attachment.
    Initiating Events Cornerstone
   
    *   Unplanned Scrams per 7000 Critical Hours (January 2008 to December 2008)
No findings of significance were identified.  
    *   Unplanned Transients per 7000 Critical Hours (January 2008 to December 2008)
    The inspectors reviewed data and plant records from January 2008 to December 2008.
4.  
    The records included PI data summary reports, licensee event reports, operator
OTHER ACTIVITIES [OA]  
    narrative logs, Entergys corrective action program, and Maintenance Rule records. The
    inspectors verified the accuracy of the number of critical hours reported, and interviewed
4OA1 Performance Indicator Verification (71151 - 3 samples)  
    the system engineers and operators responsible for data collection and evaluation.
   
    Barrier Integrity Cornerstone
  a.  
    *   RCS Activity (January 2008 to December 2008)
Inspection Scope  
    The inspectors reviewed data and plant records from January 2008 to December 2008.
    The records included performance indicator data summary reports, licensee event
The inspectors reviewed performance indicator data for the cornerstones listed below  
    reports, operator narrative logs, Entergys corrective action program, and Maintenance
and used Nuclear Energy Institute 99-02, Regulatory Assessment Performance  
    Rule records. The inspectors verified the accuracy of the number of critical hours
Indicator Guideline, Revision 5, to verify individual performance indicator accuracy and  
    reported, and interviewed the system engineers and operators responsible for data
completeness. The documents reviewed during this inspection are listed in the  
    collection and evaluation.
Attachment.  
                                                                                      Enclosure
Initiating Events Cornerstone  
*  
Unplanned Scrams per 7000 Critical Hours (January 2008 to December 2008)  
*  
Unplanned Transients per 7000 Critical Hours (January 2008 to December 2008)  
The inspectors reviewed data and plant records from January 2008 to December 2008.
The records included PI data summary reports, licensee event reports, operator  
narrative logs, Entergys corrective action program, and Maintenance Rule records. The  
inspectors verified the accuracy of the number of critical hours reported, and interviewed  
the system engineers and operators responsible for data collection and evaluation.  
Barrier Integrity Cornerstone  
*  
RCS Activity (January 2008 to December 2008)  
The inspectors reviewed data and plant records from January 2008 to December 2008.
The records included performance indicator data summary reports, licensee event  
reports, operator narrative logs, Entergys corrective action program, and Maintenance  
Rule records. The inspectors verified the accuracy of the number of critical hours  
reported, and interviewed the system engineers and operators responsible for data  
collection and evaluation.  


                                                31
31  
   b.  Findings
Enclosure 
      No findings of significance were identified.
   b.  
4OA2 Identification and Resolution of Problems (71152)
Findings
.1   Routine Problem Identification & Resolution Program Review
   a. Inspection Scope
   
      As required by Inspection Procedure 71152, Identification and Resolution of Problems,
No findings of significance were identified.  
      and to identify repetitive equipment failures or specific human performance issues for
       
      follow-up, the inspectors performed a daily screening of all items entered into Entergys
4OA2 Identification and Resolution of Problems (71152)  
      corrective action program. The review was accomplished by accessing Entergys
      computerized database for condition reports, and attending condition report screening
.1  
      meetings.
Routine Problem Identification & Resolution Program Review  
      In accordance with the baseline inspection modules, the inspectors selected corrective
 
      action program items across the Initiating Events, Mitigating Systems, and Barrier
   a.  
      Integrity cornerstones for further follow-up and review. The inspectors assessed
Inspection Scope  
      Entergys threshold for problem identification, adequacy of the causal analysis, extent of
      condition reviews, and operability determinations, and timeliness of the associated
As required by Inspection Procedure 71152, Identification and Resolution of Problems,  
      corrective actions. The condition reports reviewed during this inspection are listed in the
and to identify repetitive equipment failures or specific human performance issues for  
      Attachment.
follow-up, the inspectors performed a daily screening of all items entered into Entergys  
   b.  Findings
corrective action program. The review was accomplished by accessing Entergys  
      No findings of significance were identified
computerized database for condition reports, and attending condition report screening  
4OA3 Event Followup
meetings.  
.1   Condensate Return Line Leak on February 15, 2009
  a.   Inspection Scope
In accordance with the baseline inspection modules, the inspectors selected corrective  
    On February 15, 2009, an operator observed indications of wetness in a pipe sleeve in
action program items across the Initiating Events, Mitigating Systems, and Barrier  
    the floor of the auxiliary feed pump building. The operator notified the control room.
Integrity cornerstones for further follow-up and review. The inspectors assessed  
    Chemistry samples of the water were drawn and analyzed. On February 16, Entergy
Entergys threshold for problem identification, adequacy of the causal analysis, extent of  
    determined the chemistry results indicated the water was from the condensate storage
condition reviews, and operability determinations, and timeliness of the associated  
    tank (CST) return line. The inspectors reviewed the technical specifications (TS) to
corrective actions. The condition reports reviewed during this inspection are listed in the  
    determine whether operators entered the applicable TS action statements for the CST
Attachment.  
    and completed required actions to administratively determine the back-up on-site city
    water tank was available, if needed, to provide water to the auxiliary feedwater pumps.
   b.  
    The inspectors reviewed Entergys operability evaluation of the CST to determine
Findings
    whether it was technically supported. In addition, the inspectors reviewed the impact of
   
    the leak on the auxiliary feed water system which utilizes the CST as a primary source of
No findings of significance were identified
    water and circulates water back to the CST through the CST return piping. The
    inspectors also reviewed chemistry and radiological samples taken of the water to assess
4OA3 Event Followup  
    the environmental impact of the leak and determine if the release was below NRC
    regulatory limits for liquid effluents.
.1  
                                                                                        Enclosure
Condensate Return Line Leak on February 15, 2009  
   
a.  
Inspection Scope  
On February 15, 2009, an operator observed indications of wetness in a pipe sleeve in  
the floor of the auxiliary feed pump building. The operator notified the control room.
Chemistry samples of the water were drawn and analyzed. On February 16, Entergy  
determined the chemistry results indicated the water was from the condensate storage  
tank (CST) return line. The inspectors reviewed the technical specifications (TS) to  
determine whether operators entered the applicable TS action statements for the CST  
and completed required actions to administratively determine the back-up on-site city  
water tank was available, if needed, to provide water to the auxiliary feedwater pumps.
The inspectors reviewed Entergys operability evaluation of the CST to determine  
whether it was technically supported. In addition, the inspectors reviewed the impact of  
the leak on the auxiliary feed water system which utilizes the CST as a primary source of  
water and circulates water back to the CST through the CST return piping. The  
inspectors also reviewed chemistry and radiological samples taken of the water to assess  
the environmental impact of the leak and determine if the release was below NRC  
regulatory limits for liquid effluents.  


                                              32
32  
  b. Findings and Observations
Enclosure  
    No findings of significance were identified.
b.  
      Entergy excavated a portion of the CST piping in the area of the identified leakage and
Findings and Observations  
      determined that the CST return pipe was leaking due to a hole the pipe where a small
      area of a protective coating was missing. Entergy also identified two additional areas of
No findings of significance were identified.  
      piping with metal loss that did not exceed ASME Code minimum required wall thickness.
      However, the areas were repaired while the opportunity existed. Entergy removed the
Entergy excavated a portion of the CST piping in the area of the identified leakage and  
      portion of pipe with the localized defects and sent the specimen to a laboratory for
determined that the CST return pipe was leaking due to a hole the pipe where a small  
      analysis to identify the causes. The inspectors determined that the actions Entergy
area of a protective coating was missing. Entergy also identified two additional areas of  
      implemented to evaluate and repair the leaking CST pipe to restore operability to the
piping with metal loss that did not exceed ASME Code minimum required wall thickness.
      CST were adequate and in accordance with their operating license. Additionally, the
However, the areas were repaired while the opportunity existed. Entergy removed the  
      inspectors determined that the evaluations and actions Entergy performed to evaluate
portion of pipe with the localized defects and sent the specimen to a laboratory for  
      and maintain operability of the auxiliary feed pumps were adequate. Entergy analyzed
analysis to identify the causes. The inspectors determined that the actions Entergy  
      the water leaking up through the sleeve and determined it was CST water based on
implemented to evaluate and repair the leaking CST pipe to restore operability to the  
      hydrazine and tritium levels. The amount of tritium detected in the water was consistent
CST were adequate and in accordance with their operating license. Additionally, the  
      with that found in the CST, for example, analyses of samples of water from the leak
inspectors determined that the evaluations and actions Entergy performed to evaluate  
      returned 2000 - 2300 picocuries per liter (pCi/l). The release was determined to be
and maintain operability of the auxiliary feed pumps were adequate. Entergy analyzed  
      below the NRC regulatory limits for liquid effluents. For added perspective, while not
the water leaking up through the sleeve and determined it was CST water based on  
      drinking water, the Environmental Protection Agency environmental limit for drinking
hydrazine and tritium levels. The amount of tritium detected in the water was consistent  
      water requires tritium levels less than 20,000 pCi/l.
with that found in the CST, for example, analyses of samples of water from the leak  
      Entergy initiated a root cause analysis to determine causes of the leak that is scheduled
returned 2000 - 2300 picocuries per liter (pCi/l). The release was determined to be  
      to be completed in May 2009. At the end of the inspection period, the inspectors were
below the NRC regulatory limits for liquid effluents. For added perspective, while not  
      monitoring the performance of Entergy in implementing its corrective action program to
drinking water, the Environmental Protection Agency environmental limit for drinking  
      address the issue and develop a root cause evaluation and further corrective actions.
water requires tritium levels less than 20,000 pCi/l.  
4OA5 Other Activities
.1   Continued Groundwater Sampling Effort to Monitor Tritium (Deviation Memorandum
Entergy initiated a root cause analysis to determine causes of the leak that is scheduled  
    Inspection)
to be completed in May 2009. At the end of the inspection period, the inspectors were  
  a. Inspection Scope
monitoring the performance of Entergy in implementing its corrective action program to  
    During the week of March 23-27, 2009, the inspectors met with Entergy representatives
address the issue and develop a root cause evaluation and further corrective actions.  
    to review the results of recent groundwater samples, as well as those taken and
    analyzed in 2008. The review was conducted against criteria contained in 10CFR20,
4OA5 Other Activities  
    10CFR50, and applicable industry standards.
    The review of the data included a comparison of Entergys data with split samples taken
.1  
    by the NRC of monitoring wells MW-66 and MW-67, as well as the LaFarge sample
Continued Groundwater Sampling Effort to Monitor Tritium (Deviation Memorandum  
    point. In all, 47 samples were analyzed and compared from January 2008 through
Inspection)  
    January 2009. Isotopic analyses were performed and compared at each of the sample
   
    points for: Tritium, Strontium 90, Nickel 63, and gamma emitters such as Cobalt-60 and
a.  
    Cesium-137. Results of the NRC samples can be found in ADAMS accession numbers:
Inspection Scope  
    ML081420676, ML082690244, ML082690202, ML082690237, ML082730830,
    ML082730810, ML090400523, ML090400516, ML090400502, ML090923932,
During the week of March 23-27, 2009, the inspectors met with Entergy representatives  
    ML090920949.
to review the results of recent groundwater samples, as well as those taken and  
                                                                                      Enclosure
analyzed in 2008. The review was conducted against criteria contained in 10CFR20,  
10CFR50, and applicable industry standards.  
The review of the data included a comparison of Entergys data with split samples taken  
by the NRC of monitoring wells MW-66 and MW-67, as well as the LaFarge sample  
point. In all, 47 samples were analyzed and compared from January 2008 through  
January 2009. Isotopic analyses were performed and compared at each of the sample  
points for: Tritium, Strontium 90, Nickel 63, and gamma emitters such as Cobalt-60 and  
Cesium-137. Results of the NRC samples can be found in ADAMS accession numbers:
ML081420676, ML082690244, ML082690202, ML082690237, ML082730830,  
ML082730810, ML090400523, ML090400516, ML090400502, ML090923932,  
ML090920949.  


                                              33
33  
    Entergy=s evaluation of recent groundwater results are documented in condition reports:
Enclosure 
    CR-IP2-2009-00883, CR-IP2-2009-01110, CR-IP2-2009-01111, CR-IP2-2009-01113,
Entergy=s evaluation of recent groundwater results are documented in condition reports:
    and CR-IP2-2009-01114.
CR-IP2-2009-00883, CR-IP2-2009-01110, CR-IP2-2009-01111, CR-IP2-2009-01113,  
   b. Findings
and CR-IP2-2009-01114.  
    No findings of significance were identified.
    The inspectors concluded that overall, there was agreement between Entergy
   b.  
    personnels results and those independently analyzed by the NRC, and that actions
Findings  
    taken by Entergy have been appropriate. The inspectors also noted that conservative
    estimates indicate that the samples represent a very small fraction of the permissible
No findings of significance were identified.  
    public dose limits and are negligible with respect to natural background radiation levels.
.2   Quarterly Resident Inspector Observations of Security Personnel and Activities
The inspectors concluded that overall, there was agreement between Entergy  
   a. Inspection Scope
personnels results and those independently analyzed by the NRC, and that actions  
    During the inspection period, the inspectors conducted observations of security force
taken by Entergy have been appropriate. The inspectors also noted that conservative  
    personnel and activities to ensure that these activities were consistent with Entergy
estimates indicate that the samples represent a very small fraction of the permissible  
    security procedures and applicable regulatory requirements. Although these
public dose limits and are negligible with respect to natural background radiation levels.  
    observations did not constitute additional inspection samples, the inspections were
    considered an integral part of the normal, resident inspector plant status reviews during
.2  
    implementation of the baseline inspection program.
Quarterly Resident Inspector Observations of Security Personnel and Activities  
   b. Findings
    No findings of significance were identified.
   a.  
4OA6 Meetings
Inspection Scope  
    Exit Meeting Summary
    On April 15, 2009, the inspectors presented the inspection results to Joe Pollock and
During the inspection period, the inspectors conducted observations of security force  
    other Entergy staff members, who acknowledged the inspection results presented.
personnel and activities to ensure that these activities were consistent with Entergy  
    Entergy did not identify any material as proprietary.
security procedures and applicable regulatory requirements. Although these  
ATTACHMENT: SUPPLEMENTAL INFORMATION
observations did not constitute additional inspection samples, the inspections were  
                                                                                      Enclosure
considered an integral part of the normal, resident inspector plant status reviews during  
implementation of the baseline inspection program.  
   b.  
Findings  
No findings of significance were identified.  
4OA6 Meetings  
Exit Meeting Summary
On April 15, 2009, the inspectors presented the inspection results to Joe Pollock and  
other Entergy staff members, who acknowledged the inspection results presented.
Entergy did not identify any material as proprietary.  
ATTACHMENT: SUPPLEMENTAL INFORMATION  


                                            A-1
A-1  
                            SUPPLEMENTAL INFORMATION
                                KEY POINTS OF CONTACT
Attachment
Entergy Personnel
J. Pollock,  Site Vice President
A. Vitale,   General Manager, Plant Operations
SUPPLEMENTAL INFORMATION  
P. Conroy,   Director of Nuclear Safety Assurance
A. Williams, Site Operations Manager
KEY POINTS OF CONTACT  
B. Sullivan, Emergency Planning Manager
S. Verrochi, System Engineering Manager
Entergy Personnel  
R. Walpole,  Licensing Manager
D. Loope,   Manager, Radiation Protection
J. Pollock,   
                  LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Site Vice President  
Opened and Closed
A. Vitale,
05000247/2009002-01               FIN           Failure to Identify Open Louvers in 11 Fire
General Manager, Plant Operations  
                                                Pump House (Section 1R01)
P. Conroy,
05000247/2009002-02             NCV             Failure to Identify Damaged Components in
Director of Nuclear Safety Assurance  
                                                EDG Ventilation Motor Control Center #2
A. Williams, Site Operations Manager  
                                                (Section 1R05)
B. Sullivan,
05000247/2009002-03             NCV             Failure to identify and Promptly Correct
Emergency Planning Manager  
                                                Degraded 480 Volt Switchgear Room Fire
S. Verrochi, System Engineering Manager  
                                                Door (Section 1R05)
R. Walpole,   
05000247/2009002-04             NCV             Inadequate Maintenance Procedure for
Licensing Manager  
                                                EDG Ventilation Motor Control Center #2
D. Loope,  
                                                (Section 1R12)
Manager, Radiation Protection  
05000247/2009002-05             NCV             Failure to Include RWST Level
                                                Maintenance In Online Risk Assessment
                                                (Section 1R13)
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
05000247/2009002-06             NCV             Inadequate Test Acceptance Criteria for
                                                Auxiliary Component Cooling Check Valves
Opened and Closed  
                                                (Section 1R22)
05000247/2009002-07             NCV             Failure to Follow Radiation Protection
05000247/2009002-01                   FIN  
                                                Procedures (Section 2OS1)
Failure to Identify Open Louvers in 11 Fire  
                                                                                  Attachment
Pump House (Section 1R01)  
05000247/2009002-02                   NCV  
Failure to Identify Damaged Components in  
EDG Ventilation Motor Control Center #2  
(Section 1R05)  
05000247/2009002-03                   NCV  
Failure to identify and Promptly Correct  
Degraded 480 Volt Switchgear Room Fire  
Door (Section 1R05)  
05000247/2009002-04                   NCV  
Inadequate Maintenance Procedure for  
EDG Ventilation Motor Control Center #2  
(Section 1R12)  
05000247/2009002-05                   NCV  
Failure to Include RWST Level  
Maintenance In Online Risk Assessment  
(Section 1R13)  
05000247/2009002-06                   NCV  
Inadequate Test Acceptance Criteria for  
Auxiliary Component Cooling Check Valves  
(Section 1R22)  
05000247/2009002-07
NCV
Failure to Follow Radiation Protection  
Procedures (Section 2OS1)  


                                              A-2
A-2  
                              LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
Attachment 
Procedures
OAP-048, Rev. 4, Seasonal Weather Preparation
LIST OF DOCUMENTS REVIEWED  
OAP-008, Rev. 5, Severe Weather Preparations
2-AOP-SSD-1, Rev. 13, Control Room Inaccessibility Safe Shutdown Control
Section 1R01: Adverse Weather Protection  
OAP-017, Rev. 5, Plant Surveillance and Operator Rounds
EN-OP-115, Rev. 5, Conduct of Operations
Procedures  
Condition Reports
OAP-048, Rev. 4, Seasonal Weather Preparation  
IP2-2009-00197         IP2-2009-00207       IP2-2009-00208         IP2-2009-00211
OAP-008, Rev. 5, Severe Weather Preparations  
IP2-2009-00212         IP2-2009-00214       IP2-2009-00215         IP2-2009-00226
2-AOP-SSD-1, Rev. 13, Control Room Inaccessibility Safe Shutdown Control  
Orders
OAP-017, Rev. 5, Plant Surveillance and Operator Rounds  
00152922       00153082       00153083       00179583
EN-OP-115, Rev. 5, Conduct of Operations  
Section 1R04: Equipment Alignment
Procedures
Condition Reports  
2-PT-M103, Rev. 2, Auxiliary Feedwater System Monthly Alignment Verification
IP2-2009-00197  
2-COL-4.1.1, Rev. 22, Component Cooling System
IP2-2009-00207  
Section 1R05: Fire Protection
IP2-2009-00208  
Procedures
IP2-2009-00211  
SAO-703, Rev. 25, Fire Protection Impairment Criteria and Surveillance
IP2-2009-00212  
EN-DC-161, Rev. 2, Control of Combustibles
IP2-2009-00214  
OAP-037, Rev. 2, Operations Electrical Equipment Operating Guidelines
IP2-2009-00215  
IP-SMM-IS-103, Rev. 0, IPEC Site Management Manual Electrical Safety
IP2-2009-00226  
2-PT-SA020, Rev. 0, Swing Fire Doors
Condition Reports
Orders  
IP2-2009-00904         IP2-2009-00526       IP2-2009-00680         IP2-2009-00709
00152922  
IP2-2009-00834         IP2-2009-00342       IP2-2009-00483         IP2-2004-05336
00153082  
IP2-2007-03561         IP2-2007-04645       IP2-2008-05447
00153083  
Orders
00179583  
51645822       51676572
Miscellaneous
Section 1R04: Equipment Alignment  
Indian Point Nuclear Generating Station, Unit 2, Fire Protection Program Plan, Rev. 9
Indian Point Pre-Fire Plans Unit 2 - Nuclear
Procedures  
IP2-RPT-03-00015, IP2 Fire Hazards Analysis, Rev. 3
2-PT-M103, Rev. 2, Auxiliary Feedwater System Monthly Alignment Verification  
1R07: Heat Sink Performance
2-COL-4.1.1, Rev. 22, Component Cooling System  
Procedures
SEP-SW-001, NRC Generic Letter 89-13 Service Water Program
Section 1R05: Fire Protection  
PT-2Y10B, 22 CCW HX Test
2-HTX-004-CCW, Component Cooling Water Heat Exchanger Maintenance
Procedures  
                                                                                    Attachment
SAO-703, Rev. 25, Fire Protection Impairment Criteria and Surveillance  
EN-DC-161, Rev. 2, Control of Combustibles  
OAP-037, Rev. 2, Operations Electrical Equipment Operating Guidelines  
IP-SMM-IS-103, Rev. 0, IPEC Site Management Manual Electrical Safety  
2-PT-SA020, Rev. 0, Swing Fire Doors  
Condition Reports  
IP2-2009-00904  
IP2-2009-00526  
IP2-2009-00680  
IP2-2009-00709  
IP2-2009-00834  
IP2-2009-00342  
IP2-2009-00483  
IP2-2004-05336  
IP2-2007-03561  
IP2-2007-04645  
IP2-2008-05447  
Orders  
51645822  
51676572  
Miscellaneous  
Indian Point Nuclear Generating Station, Unit 2, Fire Protection Program Plan, Rev. 9  
Indian Point Pre-Fire Plans Unit 2 - Nuclear  
IP2-RPT-03-00015, IP2 Fire Hazards Analysis, Rev. 3  
1R07: Heat Sink Performance  
Procedures  
SEP-SW-001, NRC Generic Letter 89-13 Service Water Program  
PT-2Y10B, 22 CCW HX Test  
2-HTX-004-CCW, Component Cooling Water Heat Exchanger Maintenance  


                                                A-3
A-3  
Work Orders
51675733
Attachment 
Condition Reports
Work Orders  
IP2-2005-0673         IP2-2005-0768           IP2-2005-1268     IP2-2006-7126
51675733  
IP2-2006-3974
Miscellaneous
Condition Reports  
EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines
IP2-2005-0673  
Preliminary Report of Eddy Current Testing dated 2/10/09
IP2-2005-0768  
21 CCW Hx Inspection Reports dated 2/23/2005 and 1/8/2007
IP2-2005-1268  
22 CCW Hx Inspection Reports dated 2/23/2005 and 12/12/2006
IP2-2006-7126  
Section 1R11: Licensed Operator Requalification Program
Procedures
IP2-2006-3974  
OAP-033, Conduct of Operations Simulator Training, Evaluations, and Debriefs, Rev. 4
OAP-032, Operations Training Program, Rev. 9
Miscellaneous  
2-E-0, Rev. 0, Reactor Trip or Safety Injection
EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines  
2-ECA-0.0, Rev. 3, Loss of All AC Power
Preliminary Report of Eddy Current Testing dated 2/10/09  
2-AOP-480V-1, Rev. 5, Loss of Normal Power to any 480V Bus
21 CCW Hx Inspection Reports dated 2/23/2005 and 1/8/2007  
Miscellaneous
22 CCW Hx Inspection Reports dated 2/23/2005 and 12/12/2006  
LRQ-SES-21, Rev. 0, IPEC Evalauted Scenario for Loss of All AC Power
Section 1R12: Maintenance Effectiveness
Section 1R11: Licensed Operator Requalification Program  
Procedures
2-MCC-003-ELC, Rev 0, Klockner-Moeller, Series 200, 480 Volt Motor Control Center
Procedures  
    Preventive Maintenance
OAP-033, Conduct of Operations Simulator Training, Evaluations, and Debriefs, Rev. 4  
2-PC-Q2, Rev. 19, Refueling Water Storage Tank Level
OAP-032, Operations Training Program, Rev. 9  
0-MS-412, Rev. 0, Inspection and Cleaning of Bus Bars, Contacts, Ground Connections, Wiring
2-E-0, Rev. 0, Reactor Trip or Safety Injection  
    and Insulators
2-ECA-0.0, Rev. 3, Loss of All AC Power  
IP-SMM-IS-103, Rev. 0, IPEC Site Management Manual Electrical Safety
2-AOP-480V-1, Rev. 5, Loss of Normal Power to any 480V Bus  
0-GNR-404-ELC, Rev. 1, Emergency Diesel Generator 2-Year Inspection
2-GNR-015-ELC, Rev. 2, Emergency Diesel Generator Preventive Maintenance 2-Year
Miscellaneous  
2-PT-M021B, Rev. 17, Emergency Diesel Generator 22 Load Test
LRQ-SES-21, Rev. 0, IPEC Evalauted Scenario for Loss of All AC Power  
Condition Reports
IP2-2009-00527       IP2-2009-00532         IP2-2009-01041     IP2-2003-00948
Section 1R12: Maintenance Effectiveness  
IP2-2009-00342       IP2-2009-00483         IP2-2004-03106     IP2-2007-01893
IP2-2008-05382       IP2-2009-00486         IP2-2009-00041     IP2-2009-00178
Procedures  
IP2-2006-04101       IP2-2009-00093         IP2-2007-03476     IP2-2007-04921
2-MCC-003-ELC, Rev 0, Klockner-Moeller, Series 200, 480 Volt Motor Control Center  
IP2-2008-00454       IP2-2008-00907         IP2-2008-03976
Preventive Maintenance  
Orders
2-PC-Q2, Rev. 19, Refueling Water Storage Tank Level  
51557262       51676147       06-16146       51696697     51322921     51268313
0-MS-412, Rev. 0, Inspection and Cleaning of Bus Bars, Contacts, Ground Connections, Wiring  
00181009       00167536       04-26645       57696714     51649505     51654261
and Insulators  
00118733       07-03476       07-04921       08-00454     08-00907     09-00532
IP-SMM-IS-103, Rev. 0, IPEC Site Management Manual Electrical Safety  
Drawing
0-GNR-404-ELC, Rev. 1, Emergency Diesel Generator 2-Year Inspection  
309030-02, Loop diagram RWST level indication
2-GNR-015-ELC, Rev. 2, Emergency Diesel Generator Preventive Maintenance 2-Year  
3WS-463-610-14-20101-3, Schematic for EDG HVAC Heater
2-PT-M021B, Rev. 17, Emergency Diesel Generator 22 Load Test  
                                                                                  Attachment
Condition Reports  
IP2-2009-00527  
IP2-2009-00532  
IP2-2009-01041  
IP2-2003-00948  
IP2-2009-00342  
IP2-2009-00483  
IP2-2004-03106  
IP2-2007-01893  
IP2-2008-05382  
IP2-2009-00486  
IP2-2009-00041  
IP2-2009-00178  
IP2-2006-04101  
IP2-2009-00093  
IP2-2007-03476  
IP2-2007-04921  
IP2-2008-00454  
IP2-2008-00907  
IP2-2008-03976  
Orders  
51557262  
51676147  
06-16146  
51696697  
51322921  
51268313  
00181009  
00167536  
04-26645  
57696714  
51649505  
51654261  
00118733  
07-03476  
07-04921  
08-00454  
08-00907  
09-00532  
Drawing  
309030-02, Loop diagram RWST level indication  
3WS-463-610-14-20101-3, Schematic for EDG HVAC Heater  


                                              A-4
A-4  
IP2-S-000231-04, Schematic for EDG Building Ventilation Distribution
B248513-12, 480V MCC 26C and CCR Ventilation Distribution
Attachment 
B228434-02, Class A Boundary for Electrical Systems
IP2-S-000231-04, Schematic for EDG Building Ventilation Distribution  
Miscellaneous
B248513-12, 480V MCC 26C and CCR Ventilation Distribution  
Maintenance Rule Basis Document Residual Heat Removal System, dated 5/23/05
B228434-02, Class A Boundary for Electrical Systems  
Maintenance Rule Basis Document HVAC Emergency Diesel Building, dated 5/23/05
IP-SMM-AD-102, Att 10.2, dated 4/6/08, for revision to procedure 2-MCC-003-ELC
Miscellaneous  
Vendor Manual, Klockner-Moeller Series 200 Motor Control Center
Maintenance Rule Basis Document Residual Heat Removal System, dated 5/23/05  
Vendor Manual, Qmark MUH Series Modular Unit Heaters
Maintenance Rule Basis Document HVAC Emergency Diesel Building, dated 5/23/05  
Vendor Manual, ALCO Fuel Injection Nozzle and Holder
IP-SMM-AD-102, Att 10.2, dated 4/6/08, for revision to procedure 2-MCC-003-ELC  
Maintenance Rule Expert Panel Meeting Minutes dated 2/14/05
Vendor Manual, Klockner-Moeller Series 200 Motor Control Center  
Tagout 2-480V-Panel-MCC26C dated 4/3/08
Vendor Manual, Qmark MUH Series Modular Unit Heaters  
DRN-08-01336 dated 4/6/08 for procedure 2-MCC-003-ELC
Vendor Manual, ALCO Fuel Injection Nozzle and Holder
PMCR ER-06-33534, to establish maintenance activity for EDG HVAC MCC
Maintenance Rule Expert Panel Meeting Minutes dated 2/14/05  
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Tagout 2-480V-Panel-MCC26C dated 4/3/08  
Procedures
DRN-08-01336 dated 4/6/08 for procedure 2-MCC-003-ELC  
IP-SMM-WM-101, On-Line Risk Assessment
PMCR ER-06-33534, to establish maintenance activity for EDG HVAC MCC  
2-PC-Q109, Recalibration of Nis and OT/OP delta T parameters
PT-Q17A, Verify ASSS supply to 21 AFP
Section 1R13: Maintenance Risk Assessments and Emergent Work Control  
2-PT-Q027A, 21 Auxiliary Feed Pump
2-PC-Q2, Rev. 19, Refueling Water Storage Tank Level
Procedures  
2-ES-1.3, Rev. 2, Transfer to Cold Leg Recirculation
IP-SMM-WM-101, On-Line Risk Assessment  
Condition Reports
2-PC-Q109, Recalibration of Nis and OT/OP delta T parameters  
IP2-2009-00018       IP2-2009-00027       IP2-2009-00139       IP2-2009-00143
PT-Q17A, Verify ASSS supply to 21 AFP  
IP2-2009-00148       IP2-2009-00389
2-PT-Q027A, 21 Auxiliary Feed Pump  
Work Orders
2-PC-Q2, Rev. 19, Refueling Water Storage Tank Level  
00165604     51654961       51692571     51692351       51696697
2-ES-1.3, Rev. 2, Transfer to Cold Leg Recirculation  
Miscellaneous
Equipment Out-Of-Service (EOOS) risk assessment reports
Condition Reports  
Section 1R15: Operability Evaluations
IP2-2009-00018  
Procedures
IP2-2009-00027  
2-PT-Q031A, 21 Auxiliary Component Cooling Pump
IP2-2009-00139  
2-PT-Q031B, 22 Auxiliary Component Cooling Pump
IP2-2009-00143  
EN-MA-133, Control of Scaffolding
IP2-2009-00148  
2-AOP-IB-1, Loss of Power to an Instrument Bus
IP2-2009-00389  
2-PT-M021B, Rev. 17, Emergency Diesel Generator 22 Load Test
2-SOP-AFW-002, Rev. 1, Auxiliary Feedwater System Operation Support Procedure
Work Orders  
Drawings
00165604  
A249955-21, 480V AC MCC 29 & 29A
51654961  
Calculation
51692571  
IP3-CALC-FW-01482, Rev. 0, Feedwater Stratification and Auxiliary Feedwater
51692351  
                                                                                Attachment
51696697  
Miscellaneous  
Equipment Out-Of-Service (EOOS) risk assessment reports  
Section 1R15: Operability Evaluations  
Procedures  
2-PT-Q031A, 21 Auxiliary Component Cooling Pump  
2-PT-Q031B, 22 Auxiliary Component Cooling Pump  
EN-MA-133, Control of Scaffolding  
2-AOP-IB-1, Loss of Power to an Instrument Bus  
2-PT-M021B, Rev. 17, Emergency Diesel Generator 22 Load Test  
2-SOP-AFW-002, Rev. 1, Auxiliary Feedwater System Operation Support Procedure  
Drawings  
A249955-21, 480V AC MCC 29 & 29A  
Calculation  
IP3-CALC-FW-01482, Rev. 0, Feedwater Stratification and Auxiliary Feedwater  


                                              A-5
A-5  
Condition Reports
IP2-2009-0500           IP2-2009-0505       IP2-2008-3749       IP2-2009-0547
Attachment 
IP2-2009-0567           IP2-2009-0509       IP2-2005-0252       IP2-2009-0552
Condition Reports  
IP2-2009-0655           IP2-2008-2705       IP2-2009-0041       IP2-2009-0093
IP2-2009-0500  
Work Orders
IP2-2009-0505  
NP-99-07694
IP2-2008-3749  
Miscellaneous
IP2-2009-0547  
WCAP-12312, Rev. 2, Safety Evaluation for an Ultimate Heat Sink Temperature Increase to 95F
IP2-2009-0567  
  at Indian Point Unit 2
IP2-2009-0509  
Heat exchanger data sheet for containment recirculation pump number 22 motor cooler
IP2-2005-0252  
WCAP-7829, Fan Cooler Motor Unit Test
IP2-2009-0552  
Environmental Qualification Report for Containment Recirculation Pump Motors
IP2-2009-0655  
IP2-CCW-DBD, Component Cooling Water design bases document
IP2-2008-2705  
IP2-DBD-207, Design Basis Document for 118V AC Electrical System
IP2-2009-0041  
AMSE OM-2001 Edition
IP2-2009-0093  
Unit 2 active scaffold list
VM 1073-1.2, Vendor manual for auxiliary component cooling pumps
Work Orders  
VM 1100, vendor manual for 118V AC solid state static inverters
NP-99-07694  
Work order NP-89-43777, replacement of 22 ACCP impeller
IP2-AFW-DBD, Rev. 1, AFW Design Basis Document
Miscellaneous  
Section 1R18: Plant Modifications
WCAP-12312, Rev. 2, Safety Evaluation for an Ultimate Heat Sink Temperature Increase to 95F  
Procedures
at Indian Point Unit 2  
2-SOP-18-1, Main and Reheat Steam System
Heat exchanger data sheet for containment recirculation pump number 22 motor cooler  
TP-SQ-11.016, Post Work Test Program (historical)
WCAP-7829, Fan Cooler Motor Unit Test  
Condition Reports
Environmental Qualification Report for Containment Recirculation Pump Motors  
IP2-2009-0983           IP2-2009-0137       IP2-2008-5636       IP2-2009-0077
IP2-CCW-DBD, Component Cooling Water design bases document  
IP2-2009-0069           IP2-2009-0062       IP2-2008-5621       IP2-2009-0781
IP2-DBD-207, Design Basis Document for 118V AC Electrical System  
Work Orders
AMSE OM-2001 Edition  
IP2-03-11725           IP2-02-32013       51305160
Unit 2 active scaffold list  
Drawings
VM 1073-1.2, Vendor manual for auxiliary component cooling pumps  
B235623-6, Atmospheric Steam Dump Panel
VM 1100, vendor manual for 118V AC solid state static inverters  
9321-F-70313, Auxiliary Boiler Feed Pump Room Instrument Piping
Work order NP-89-43777, replacement of 22 ACCP impeller  
Miscellaneous
IP2-AFW-DBD, Rev. 1, AFW Design Basis Document  
IP2 Maintenance Rule Basis for Main Steam System
IP2-MS-DBD, Design Basis Document for the Main Steam System
Section 1R18: Plant Modifications  
IPT-RPT-05-00071, Appendix R Safe Shutdown Analysis
SEE-03-5, Indian Point Unit 2 RHR Cooldown Analysis for the 5% Power Uprate
Procedures  
IP2 Inservice Testing Program Basis Data Sheets for PCV-1136 & 1137 (23/24 SG ADVs)
2-SOP-18-1, Main and Reheat Steam System  
ER 06-2-012, Install Secondary Backup Nitrogen Cylinders at both S/G ADV Local Control
TP-SQ-11.016, Post Work Test Program (historical)  
        Panels in the ABFP Building
                                                                                Attachment
Condition Reports  
IP2-2009-0983  
IP2-2009-0137  
IP2-2008-5636  
IP2-2009-0077  
IP2-2009-0069  
IP2-2009-0062  
IP2-2008-5621  
IP2-2009-0781  
Work Orders  
IP2-03-11725
IP2-02-32013
51305160  
Drawings  
B235623-6, Atmospheric Steam Dump Panel  
9321-F-70313, Auxiliary Boiler Feed Pump Room Instrument Piping
Miscellaneous  
IP2 Maintenance Rule Basis for Main Steam System  
IP2-MS-DBD, Design Basis Document for the Main Steam System  
IPT-RPT-05-00071, Appendix R Safe Shutdown Analysis  
SEE-03-5, Indian Point Unit 2 RHR Cooldown Analysis for the 5% Power Uprate  
IP2 Inservice Testing Program Basis Data Sheets for PCV-1136 & 1137 (23/24 SG ADVs)  
ER 06-2-012, Install Secondary Backup Nitrogen Cylinders at both S/G ADV Local Control  
Panels in the ABFP Building  


                                              A-6
A-6  
Section 1R19: Post-Maintenance Testing
Procedures
Attachment 
OAP-24, Operations Testing, Rev. 3
Section 1R19: Post-Maintenance Testing  
2-PT-M021C, Rev. 16, Emergency Diesel Generator 23 Load Test
0-GNR-403-ELC, Emergency Diesel Generator Quarterly Inspection
Procedures  
2-PT-Q033B, 21 Charging Pump
OAP-24, Operations Testing, Rev. 3  
2-SOP-4.1.2, Rev. 34, Component Cooling System Operation
2-PT-M021C, Rev. 16, Emergency Diesel Generator 23 Load Test  
Orders
0-GNR-403-ELC, Emergency Diesel Generator Quarterly Inspection  
51797559       51797558     52027651       00183296     00157710     51675732
2-PT-Q033B, 21 Charging Pump  
Section 1R22: Surveillance Testing
2-SOP-4.1.2, Rev. 34, Component Cooling System Operation  
Procedures
2-PT-2M4, Safety Injection System Train A Actuation Logic and Master Relay Test
Orders  
2-PT-Q013, Inservice Valve Tests
51797559  
2-PT-Q013-DS027, Valve 888A IST Data Sheet
51797558  
0-SOP-LEAKRATE-001, Rev. 1, RCS Leakrate Surveillance, Evaluation and Leak Identification
52027651  
2-PT-Q030C, Rev. 18, 23 Component Cooling Water Pump
00183296  
Drawings
00157710  
11497, Valve 888A
51675732  
Condition Reports
IP2-2007-1754         IP2-2008-1443         IP2-2008-2002       IP2-2007-3329
Section 1R22: Surveillance Testing  
Orders
51694305
Procedures  
Miscellaneous
2-PT-2M4, Safety Injection System Train A Actuation Logic and Master Relay Test  
IP2-ESF DBD, Design Basis Document for Engineered Safeguards Features System
2-PT-Q013, Inservice Valve Tests  
IP2 Inservice Testing Program Data Sheet - Valve 888A
2-PT-Q013-DS027, Valve 888A IST Data Sheet  
PGI-00066-01, 888 A & B Diff Pr Calc
0-SOP-LEAKRATE-001, Rev. 1, RCS Leakrate Surveillance, Evaluation and Leak Identification  
Section 1EP6: Drill Evaluation
2-PT-Q030C, Rev. 18, 23 Component Cooling Water Pump  
Procedures
IP-EP-120, Rev. 3, Emergency Classification
Drawings  
Miscellaneous
11497, Valve 888A  
IP-EP-115, Rev. 24, form EP-1 radiological emergency data forms dated 2/23/09
Section 2OS1: Access Control to Radiologically Significant Areas and
Condition Reports  
Section 2OS2: ALARA Planning and Controls
IP2-2007-1754  
Procedures
IP2-2008-1443  
EN-RP-100, Rev. 03, Radworker Expectations
IP2-2008-2002  
EN-RP-101, Rev. 04, Access Control for Radiologically Controlled Areas
IP2-2007-3329  
EN-RP-102, Rev. 02, Radiological Control
EN-RP-105, Rev. 04, Radiation Work Permits
Orders  
EN-RP-108, Rev. 07, Radiation Protection Posting
51694305  
EN-RP-110, Rev. 05, ALARA Program
                                                                                  Attachment
Miscellaneous  
IP2-ESF DBD, Design Basis Document for Engineered Safeguards Features System  
IP2 Inservice Testing Program Data Sheet - Valve 888A  
PGI-00066-01, 888 A & B Diff Pr Calc  
Section 1EP6: Drill Evaluation  
Procedures  
IP-EP-120, Rev. 3, Emergency Classification  
Miscellaneous  
IP-EP-115, Rev. 24, form EP-1 radiological emergency data forms dated 2/23/09  
Section 2OS1: Access Control to Radiologically Significant Areas and  
Section 2OS2: ALARA Planning and Controls  
Procedures  
EN-RP-100, Rev. 03, Radworker Expectations  
EN-RP-101, Rev. 04, Access Control for Radiologically Controlled Areas  
EN-RP-102, Rev. 02, Radiological Control  
EN-RP-105, Rev. 04, Radiation Work Permits  
EN-RP-108, Rev. 07, Radiation Protection Posting  
EN-RP-110, Rev. 05, ALARA Program  


                                              A-7
A-7  
EN-RP-121, Rev. 04, Radioactive Material Control
EN-RP-131, Rev. 06, Air Sampling
Attachment 
EN-RP-141, Rev. 04, Job Coverage
EN-RP-121, Rev. 04, Radioactive Material Control  
EN-RP-151, Rev. 02, Radiological Diving
EN-RP-131, Rev. 06, Air Sampling  
EN-RP-202, Rev. 06, Personnel Monitoring
EN-RP-141, Rev. 04, Job Coverage  
EN-RP-203, Rev. 02, Dose Assessment
EN-RP-151, Rev. 02, Radiological Diving  
EN-RP-204, Rev. 02, Special Monitoring Requirements
EN-RP-202, Rev. 06, Personnel Monitoring  
EN-RP-205, Rev. 02, Prenatal Monitoring
EN-RP-203, Rev. 02, Dose Assessment  
EN-RP-208, Rev. 02, Whole Body Counting and In-Vitro Bioassay
EN-RP-204, Rev. 02, Special Monitoring Requirements  
Condition Reports
EN-RP-205, Rev. 02, Prenatal Monitoring  
CR-IP3-2009-00752, CR-IP3-2009-00785, CR-IP3-2009-00857, CR-IP3-2009-00885
EN-RP-208, Rev. 02, Whole Body Counting and In-Vitro Bioassay  
CR-IP3-2009-00886, CR-IP3-2009-00937, CR-IP3-2009-00998, CR-IP3-2009-01006
CR-IP3-2009-01107, CR-IP3-2009-01154, CR-IP3-2009-01169, CR-IP3-2009-01171
Condition Reports  
CR-IP3-2009-01183, CR-IP3-2009-01253, CR-IP3-2009-01293, CR-IP3-2009-01295
CR-IP3-2009-00752, CR-IP3-2009-00785, CR-IP3-2009-00857, CR-IP3-2009-00885  
CR-IP3-2009-01296, CR-IP3-2009-01318, CR-IP2-2009-00883, CR-IP2-2009-01110,
CR-IP3-2009-00886, CR-IP3-2009-00937, CR-IP3-2009-00998, CR-IP3-2009-01006  
CR-IP2-2009-01111, CR-IP2-2009-01113, CR-IP2-2009-01114
CR-IP3-2009-01107, CR-IP3-2009-01154, CR-IP3-2009-01169, CR-IP3-2009-01171  
Miscellaneous
CR-IP3-2009-01183, CR-IP3-2009-01253, CR-IP3-2009-01293, CR-IP3-2009-01295  
Radiation Protection Attention Logs (Electronic Dosimeter Alarms)
CR-IP3-2009-01296, CR-IP3-2009-01318, CR-IP2-2009-00883, CR-IP2-2009-01110,
TEDE ALARA Evaluations
CR-IP2-2009-01111, CR-IP2-2009-01113, CR-IP2-2009-01114  
ALARA Committee Reviews
RP-STD-XX, Rev. X, Unreported Dosimeter Alarms and Anomolies (Draft)
Miscellaneous  
IPEC Snapshot Self-Assessment Report (IP3-LO-2007-0010) July 2007 - June 2008.
Radiation Protection Attention Logs (Electronic Dosimeter Alarms)  
RWPs: 2009-002, 2009-003, 2009-2021, 2009-3001, , 2009-3002, 2009-3056, 2009-3501,
TEDE ALARA Evaluations  
2009-3504, 2009-3515, 2009-3529
ALARA Committee Reviews  
Section 4OA1: Performance Indicator Verification
RP-STD-XX, Rev. X, Unreported Dosimeter Alarms and Anomolies (Draft)  
EN-EP-201, "Performance Indicators," Rev. 6
IPEC Snapshot Self-Assessment Report (IP3-LO-2007-0010) July 2007 - June 2008.  
EN-LI-114, Performance Indicator Process, Rev. 3
RWPs: 2009-002, 2009-003, 2009-2021, 2009-3001, , 2009-3002, 2009-3056, 2009-3501,  
NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 5
2009-3504, 2009-3515, 2009-3529  
0-CY-2765, Rev. 3, Coolant Activity Limits
Section 4OA2: Identification and Resolution of Problems
Section 4OA1: Performance Indicator Verification  
Procedures
EN-LI-102, Rev. 13, Corrective Action Process
EN-EP-201, "Performance Indicators," Rev. 6  
Condition Reports
EN-LI-114, Performance Indicator Process, Rev. 3  
IP2-2009-00342       IP2-2009-00483       IP2-2004-03106       IP2-2007-01893
NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 5  
IP2-2008-05382       IP2-2009-00486       IP2-2009-00027       IP2-2009-00139
0-CY-2765, Rev. 3, Coolant Activity Limits  
IP2-2009-00143       IP2-2009-00148
                                                                                Attachment
Section 4OA2: Identification and Resolution of Problems  
Procedures  
EN-LI-102, Rev. 13, Corrective Action Process  
Condition Reports  
IP2-2009-00342  
IP2-2009-00483  
IP2-2004-03106  
IP2-2007-01893  
IP2-2008-05382  
IP2-2009-00486
IP2-2009-00027  
IP2-2009-00139  
IP2-2009-00143  
IP2-2009-00148  


                  A-8
A-8  
        LIST OF ACRONYMS
ALARA   as low as is reasonably achievable
Attachment 
ABFW   auxiliary boiler feedwater
LIST OF ACRONYMS  
ABFP   auxiliary boiler feedwater pump
ACCP   auxiliary component cooling pump
ALARA  
ADAMS   Agency-wide Document and Management System
ASME   American Society of Mechanical Engineers
CAP     corrective action program
as low as is reasonably achievable  
CCW     component cooling water
ABFW  
CDF     core damage frequency
CFR     Code of Federal Regulations
CST     condensate storage tank
auxiliary boiler feedwater  
EDO     Executive Director of Operations
ABFP  
EDG     emergency diesel generator
ENTERGY Entergy Nuclear Northeast
EP     Emergency Preparedness
auxiliary boiler feedwater pump  
HRA     high radiation area
ACCP  
IMC     Inspection Manual Chapter
IPEC   Indian Point Energy Center
IST     in-service test
auxiliary component cooling pump  
MCC     motor control center
ADAMS  
NCV     non-cited violation
NDE     non-destructive examination
NRC     Nuclear Regulatory Commission
Agency-wide Document and Management System  
NRR     Nuclear Reactor Regulation
ASME  
NSR     non safety-related
PARS   Publicly Available Records System
PI     performance indicator
American Society of Mechanical Engineers  
RCA     radiologically controlled area
CAP  
RCS     reactor coolant system
RWP     radiation work permit
RWST   refueling water storage tank
corrective action program  
SDP     significance determination process
CCW  
SER     safety evaluation report
SG     steam generator
SR     safety related
component cooling water  
SSC     structures, systems, and components
CDF  
TS     Technical Specification
UFSAR   Updated Final Safety Evaluation Report
URI     unresolved item
core damage frequency  
WO     work order
CFR  
                                                Attachment
Code of Federal Regulations  
CST  
condensate storage tank  
EDO  
Executive Director of Operations  
EDG  
emergency diesel generator  
ENTERGY  
Entergy Nuclear Northeast  
EP  
Emergency Preparedness  
HRA  
high radiation area  
IMC  
Inspection Manual Chapter  
IPEC  
Indian Point Energy Center  
IST  
in-service test  
MCC  
motor control center  
NCV  
non-cited violation  
NDE
non-destructive examination  
NRC  
Nuclear Regulatory Commission  
NRR  
Nuclear Reactor Regulation  
NSR  
non safety-related  
PARS  
Publicly Available Records System  
PI  
performance indicator  
RCA  
radiologically controlled area  
RCS  
reactor coolant system  
RWP  
radiation work permit  
RWST  
refueling water storage tank  
SDP  
significance determination process  
SER  
safety evaluation report  
SG  
steam generator  
SR  
safety related  
SSC  
structures, systems, and components  
TS  
Technical Specification  
UFSAR  
Updated Final Safety Evaluation Report  
URI  
unresolved item  
WO  
work order
}}
}}

Latest revision as of 02:59, 12 January 2025

Entergy Pre-Filed Hearing Exhibit ENT000427, Letter from M. Gray, NRC, to J. Pollock, Entergy, Indian Point Nuclear Generating Unit 2;NRC Integrated Inspection Report 05000247/2009002
ML12090A767
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 05/14/2009
From: Mel Gray
Reactor Projects Branch 2
To: Joseph E Pollock
Entergy Nuclear Operations, Atomic Safety and Licensing Board Panel
SECY RAS
Shared Package
ML12090A727 List:
References
RAS 22156, 50-247-LR, 50-286-LR, ASLBP 07-858-03-LR-BD01 IR-09-002
Download: ML12090A767 (45)


See also: IR 05000247/2009002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

May 14, 2009

Mr. Joseph E. Pollock

Site Vice President

Entergy Nuclear Operations, Inc.

Indian Point Energy Center

450 Broadway, GSB

Buchanan, NY 10511-0249

SUBJECT:

INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED

INSPECTION REPORT 05000247/2009002

Dear Mr. Pollock:

On March 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report

documents the inspection results, which were discussed on April 15, 2009, with you and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations, and with the conditions of your

license. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

This report documents seven findings of very low safety significance (Green). Six of these

findings were also determined to be violations of NRC requirements. However, because of their

very low safety significance, and because the findings were entered into your corrective action

program, the NRC is treating these findings as non-cited violations (NCVs) consistent with

Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you

should provide a written response within 30 days of the date of this inspection report, with the

basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk,

Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director,

Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC

20555-0001; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 2.

In addition, if you disagree with the characterization of any finding, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator and the NRC Resident Inspectors at Indian Point

Nuclear Generating Unit 2. The information you provide will be considered in accordance with

Inspection Manual Chapter 0305.

ENT000427

Submitted: March 30, 2012

J. Pollock

2

In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules

of Practice, a copy of this letter, its enclosure, and your response (if any) will be available

electronically for public inspection in the NRC Public Document Room of from the Publicly

Available Records (PARS) component of the NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Mel Gray, Chief

Projects Branch 2

Division of Reactor Projects

Docket No. 50-247

License No. DPR-26

Enclosure:

Inspection Report No. 05000247/2009002

w/ Attachment: Supplemental Information

cc w/encl:

Senior Vice President, Entergy Nuclear Operations

Vice President, Operations, Entergy Nuclear Operations

Vice President, Oversight, Entergy Nuclear Operations

Senior Manager, Nuclear Safety and Licensing, Entergy Nuclear Operations

Senior Vice President and COO, Entergy Nuclear Operations

Assistant General Counsel, Entergy Nuclear Operations

Manager, Licensing, Entergy Nuclear Operations

C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law

A. Donahue, Mayor, Village of Buchanan

J. G. Testa, Mayor, City of Peekskill

R. Albanese, Four County Coordinator

S. Lousteau, Treasury Department, Entergy Services, Inc.

Chairman, Standing Committee on Energy, NYS Assembly

Chairman, Standing Committee on Environmental Conservation, NYS Assembly

Chairman, Committee on Corporations, Authorities, and Commissions

M. Slobodien, Director, Emergency Planning

P. Eddy, NYS Department of Public Service

Assemblywoman Sandra Galef, NYS Assembly

T. Seckerson, County Clerk, Westchester County Board of Legislators

A. Spano, Westchester County Executive

R. Bondi, Putnam County Executive

C. Vanderhoef, Rockland County Executive

E. A. Diana, Orange County Executive

T. Judson, Central NY Citizens Awareness Network

M. Elie, Citizens Awareness Network

Public Citizen's Critical Mass Energy Project

M. Mariotte, Nuclear Information & Resources Service

F. Zalcman, Pace Law School, Energy Project

L. Puglisi, Supervisor, Town of Cortlandt

J. Pollock

3

Congressman John Hall

Congresswoman Nita Lowey

Senator Kirsten E. Gillibrand

Senator Charles Schumer

G. Shapiro, Senator Gillibrand 's Staff

J. Riccio, Greenpeace

P. Musegaas, Riverkeeper, Inc.

M. Kaplowitz, Chairman of County Environment & Health Committee

A. Reynolds, Environmental Advocates

D. Katz, Executive Director, Citizens Awareness Network

K. Coplan, Pace Environmental Litigation Clinic

M. Jacobs, IPSEC

W. Little, Associate Attorney, NYSDEC

M. J. Greene, Clearwater, Inc.

R. Christman, Manager Training and Development

J. Spath, New York State Energy Research, SLO Designee

F. Murray, President & CEO, New York State Energy Research

A. J. Kremer, New York Affordable Reliable Electricity Alliance (NY AREA)

J. Pollock

4

In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules

of Practice, a copy of this letter, its enclosure, and your response (if any) will be available

electronically for public inspection in the NRC Public Document Room of from the Publicly

Available Records (PARS) component of the NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Mel Gray, Chief

Projects Branch 2

Division of Reactor Projects

Distribution w/encl: (via E-mail)

S. Collins, RA

M. Dapas, DRA

D. Lew, DRP

J. Clifford, DRP

M. Gray, DRP

B. Bickett, DRP

A. Rosebrook, DRP

S. McCarver, DRP

J. Heinly, DRP

G. Malone, DRP, SRI, IP2

C. Hott, DRP, RI, IP2

D. Hochmuth, DRP, OA

S. Campbell, RI OEDO

R. Nelson, NRR

M. Kowal, NRR

J. Boska, PM, NRR

J. Hughey, NRR

D. Bearde, DRP

ROPreports@nrc.gov

Region I Docket Room (w/concurrences)

SUNSI Review Complete: ____BSB____ (Reviewers Initial)

DOCUMENT NAME: G:\\DRP\\BRANCH2\\A - INDIAN POINT 2\\INSPECTION REPORTS\\IP2 IR2009-002\\IP2

2009002 REVFINAL.DOC

After declaring this document An Official Agency Record it will be released to the Public

To Receive a copy of this document, indicate in the box: C = Copy without attachment/enclosure E = Copy with attachment/enclosure N = No copy

Office

RI/DRP

RI/DRP

RI/DRP

Name

GMalone/BSB for

BBickett/

MGray/

Date

05/14/09

05/14/09

05/14/09

OFFICAL AGENCY RECORD

1

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.:

50-247

License No.:

DPR-26

Report No.:

05000247/2009002

Licensee:

Entergy Nuclear Northeast (Entergy)

Facility:

Indian Point Nuclear Generating Unit 2

Location:

450 Broadway, GSB

Buchanan, NY 10511-0249

Dates:

January 1, 2009 through March 31, 2009

Inspectors:

G. Malone, Senior Resident Inspector, Indian Point 2

C. Hott, Resident Inspector, Indian Point 2

J. Commisky, Health Physics Inspector, Region I

Approved By:

Mel Gray, Chief

Projects Branch 2

Division of Reactor Projects

2

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ............................................................................................................... 3

REPORT DETAILS ........................................................................................................................... 8

1. REACTOR SAFETY .................................................................................................................... 8

1R01

Adverse Weather Protection ............................................................................................... 8

1R04

Equipment Alignment ....................................................................................................... 10

1R05

Fire Protection .................................................................................................................. 10

1R07

Heat Sink Performance .................................................................................................... 14

1R11

Licensed Operator Requalification Program ..................................................................... 15

1R12

Maintenance Effectiveness ............................................................................................... 15

1R13

Maintenance Risk Assessments and Emergent Work Control .......................................... 18

1R15

Operability Evaluations ..................................................................................................... 19

1R18

Plant Modifications ........................................................................................................... 20

1R19

Post-Maintenance Testing ................................................................................................ 21

1R22

Surveillance Testing ......................................................................................................... 21

1EP6

Drill Evaluation ................................................................................................................ 24

2. RADIATION SAFETY ................................................................................................................ 24

2OS1

Access Control to Radiologically Significant Areas ........................................................... 24

2OS2

ALARA Planning and Controls .......................................................................................... 28

4. OTHER ACTIVITIES .................................................................................................................. 30

4OA1

Performance Indicator Verification ................................................................................... 30

4OA2

Identification and Resolution of Problems ......................................................................... 31

4OA3

Event Followup ................................................................................................................. 31

4OA5

Other Activities ................................................................................................................. 32

4OA6

Meetings ........................................................................................................................... 33

ATTACHMENT: SUPPLEMENTAL INFORMATION .................................................................... A-1

SUPPLEMENTAL INFORMATION ............................................................................................... A-1

KEY POINTS OF CONTACT ........................................................................................................ A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ............................................................. A-1

LIST OF DOCUMENTS REVIEWED ............................................................................................ A-2

LIST OF ACRONYMS .................................................................................................................. A-8

3

Enclosure

SUMMARY OF FINDINGS

IR 05000247/2009-002; 01/01/2009 - 03/31/2009; Indian Point Nuclear Generating (Indian

Point) Unit 2; Adverse Weather Protection; Fire Protection; Maintenance Effectiveness;

Maintenance Risk Assessments; Surveillance Testing; and Radiological Access Control.

This report covered a three-month period of inspection by resident and region based inspectors.

Seven findings of very low significance (Green) were identified, six of which were also

determined to be non-cited violations (NCV). The significance of most findings is indicated by

their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process. The cross-cutting aspect for each finding was

determined using IMC 0305, Operating Reactor Assessment Program. Findings for which the

significance determination process (SDP) does not apply may be Green, or be assigned a

severity level after NRC management review. The NRCs program for overseeing safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 4, dated December 2006.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors identified a NCV of very low safety significance related to 10 CFR

50, Appendix B, Criterion XVI, Corrective Actions, because Entergy did not promptly

identify and correct an adverse condition related to an electrical fault. Specifically,

personnel did not identify a safety-related cubicle had experienced an electrical fault

prior to replacement of upstream fuses and restoration of power to the damaged cubicle.

Entergy entered the issue into the corrective action program as IP2-2009-00342 and

IP2-2009-00483, trained all operations personnel on the requirements to replace fuses

and re-energize electrical equipment, and plans to revise the operations procedure for

operating electrical equipment.

This issue was more than minor because the finding was associated with the external

factors attribute of the Initiating Events cornerstone and impacted the cornerstone

objective of limiting the likelihood of those events that upset plant stability and challenge

critical safety systems during shutdown as well as power operations. The inspectors

determined that the issue increased the likelihood of a fire in the emergency diesel

generator (EDG) building. The condition was evaluated by a Senior Reactor Analyst

utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection Significance Determination

Process. It was determined that in the event of a fire consuming the MCC, no transient

would be placed on the plant and no components required to safely shutdown the plant

would be impacted. As a result, in accordance with task 2.3.5 of Appendix F, the issue

was screened to Green.

The inspectors determined that a cross-cutting aspect was associated with this finding

in the area of human performance related to conservative decision making. Specifically,

Entergys decision-making was non-conservative related to its decisions on the process

used to identify the source of the acrid odor; re-energize the damaged electrical

equipment; and keep a damaged electrical component energized for 14 days prior to its

removal from the MCC. H.1(b) per IMC 0305] (Section 1R05)

4

Enclosure

Green. The inspectors identified a NCV of very low safety significance related to TS 5.4.1, Administrative Controls: Procedures, because Entergy did not maintain an

adequate maintenance procedure for a safety-related electrical motor control center

(MCC). Specifically, the eight-year maintenance procedure for the affected EDG

ventilation MCC did not contain an adequate method to identify high resistance

connections within the cubicle as was expected in the applicable preventative

maintenance industry template. Subsequently, a high resistance connection within the

MCC developed into a phase-to-phase electrical fault on January 28, 2009. Entergy

entered the issue into the corrective action program, scoped the affected MCC and 21

additional MCCs into the sites thermography program, and planned to revise the

maintenance procedure.

This issue was more than minor because the finding was associated with the external

factors attribute of the Initiating Events cornerstone and impacted the cornerstone

objective of limiting the likelihood of those events that upset plant stability and challenge

critical safety systems during shutdown as well as power operations. Specifically, the

high resistance connection degraded into a phase-to-phase fault and increased the

likelihood of a fire in the EDG building. The condition was evaluated by a Senior

Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection Significance

Determination Process. It was determined that in the event of a fire consuming the

MCC, no transient would be placed on the plant and no components required to safely

shutdown the plant would be impacted. As a result, in accordance with task 2.3.5 of

Appendix F, the issue was screened to Green.

The inspectors determined that the finding had a cross-cutting aspect associated with

the area of problem identification and resolution related to the use of operating

experience (OE). Specifically, Entergy personnel did not implement industry

recommended practices, or an alternate equivalent method, for identifying high

resistance connections in electrical switchgear. P.2(b) per IMC 0305] (Section 1R12)

Cornerstone: Mitigating Systems

Green. The inspectors identified a finding of very low safety significance because

Entergy personnel did not adequately implement procedure EN-LI-102, Corrective Action

Process, and promptly identify a condition adverse to quality associated with open

louvers in a fire protection pump room following pump testing on January 14, 2009. The

open louvers resulted in freezing conditions in fire protection piping located in the room

and cracked two six-inch header isolation valves on January 17, 2009. Entergy entered

the issue into the corrective action program and performed a site-wide extent-of-

condition walkdown of louvers.

The finding was more than minor because it was associated with the protection against

external factors attribute of the Mitigating Systems cornerstone and it affected the

cornerstone objective of ensuring the reliability of systems that respond to initiating

events to prevent undesirable consequences. This finding was evaluated using Phase

1 of IMC 0609 Appendix F, Fire Protection Significance Determination Process. The

inspectors determined the issue was of very low safety significance (Green) because

the cracked valves were easily isolated and did not pass sufficient water to render the

fire header non-functional (low degradation rating).

5

Enclosure

The inspectors determined that the finding had a cross-cutting aspect in the area of

human performance related to work practices - human error prevention techniques.

Specifically, Entergy personnel that routinely tour the 11 fire pump house did not

question the abnormally cold room temperatures. H.4(a) per IMC 0305] (Section 1R01)

Green. The inspectors identified a NCV of very low safety significance related to License

Condition 2.K., fire protection program, because personnel did not promptly identify and

correct a degraded three-hour rated fire door latch mechanism on the west entrance of

the 480-Volt switchgear room. Specifically, inspectors identified the fire door in a non-

functional state on several instances over the course of a month. Entergy personnel

replaced the fire door latch mechanism on March 3, 2009. This issue was entered into

the corrective action program as six condition reports spanning several weeks and

included an extent of condition walkdown of site fire doors.

The finding was more than minor because it is associated with the protection against

external factors attribute of the Mitigating Systems cornerstone and affected the

cornerstone objective of ensuring the reliability of systems that respond to initiating

events to prevent undesirable consequences. This fire door, when degraded, impacts

the reliability of mitigating systems in the 480-Volt switchgear room that are relied upon

during a postulated large fire in the turbine building, and vice versa. This finding was

evaluated using Phase 1 of IMC 0609 Appendix F, Fire Protection Significance

Determination Process. Since the area in question had a fire watch posted during the

time the door was degraded for an unrelated issue, an adequate level of protection was

maintained to compensate for the degraded door. As such, according to task 1.3.1, the

inspectors determined the finding was Green.

The inspectors determined that the finding had a cross-cutting aspect in the area of

problem identification and resolution because Entergy personnel did not thoroughly

evaluate a degraded fire door latch on several occasions, such that the resolution of the

problems addressed the causes. P.1(c) per IMC 0305] (Section 1R05)

Green. The inspectors identified a NCV of very low safety significance related to 10 CFR

50.65(a)(4), because Entergy personnel did not adequately assess the risk associated

with the unavailability of the Refueling Water Storage Tank (RWST) level indication

during planned maintenance on the level transmitters and instrumentation. Entergy

entered the issue into the corrective action program (CR-IP2-2009-00342), updated the

risk model to include the maintenance activity, assessed the risk, and appropriately

coded the maintenance activity to ensure it would be risk assessed in the future.

The inspectors determined that this finding was more than minor because it was a

maintenance risk assessment issue in which personnel did not consider risk significant

SSCs that were unavailable during maintenance. The RWST level indication is

specifically listed in Table 2 of the plant specific Phase 2 SDP risk-informed inspection

notebook. The inspectors determined the significance of this issue in accordance with

IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management

Significance Determination Process. The inspectors determined that this finding was of

very low safety significance because the Incremental Core Damage Probability Deficit

was less than 1E-6.

The inspectors determined that the finding had a cross-cutting aspect in the area of

human performance related to work control. Specifically, Entergy personnel did not

6

Enclosure

appropriately plan work activities by incorporating risk insights for affected plant

equipment. H.3(a) per IMC 0305] (Section 1R13)

Green. The inspectors identified a NCV of very low safety significance related to 10

CFR 50.55a, Codes and standards, because Entergys procedure, 2-PT-Q031A for an

auxiliary component cooling water pump, did not contain appropriate acceptance criteria

for positively determining that safety-related check valves performed their safety function

when required in accordance with the American Society of Mechanical Engineers

(ASME) OM Code. Specifically, the test used reverse rotation of a parallel pump to

verify that the pumps discharge check valve was closed although previous site-specific

experience demonstrated that the pump impeller would not rotate backwards when the

check valve was stuck open. Entergy entered this issue into their corrective action

program as CR-2009-1312.

The inspectors determined that the performance deficiency was greater than minor

because it was associated with the procedure quality attribute of the Mitigating System

cornerstone and it adversely affected the cornerstones objective to ensure the reliability

of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the test criterion used in procedure 2-PT-Q013A did not ensure that valve

755A reliably performed its safety function when tested as demonstrated by testing

performed in January 2005. The inspectors determined that the performance deficiency

was of very low safety significance (Green) IMC 0609, Attachment 4, Phase 1 - Initial

Screening and Characterization of Findings. Specifically, the inspectors determined

that this finding was of very low safety significance because the finding did not result in

a loss of safety function and did not screen as potentially risk-significant due to external

events initiating events.

The inspectors determined the finding had a cross-cutting aspect related to effective

corrective actions in the corrective action program component of the problem

identification and resolution area. Specifically, Entergy personnel did not implement

effective corrective actions to resolve the testing inadequacy since 2005 and during

subsequent quarterly testing. P.1(d) per IMC 0305] (Section 1R22)

Cornerstone: Occupational Radiation Safety

Green. The inspectors identified a NCV of very low safety significance related to

Technical Specification 5.4.1.a, Procedures, because Entergy personnel did not

generate condition reports or investigation paperwork for multiple high dose-rate alarms

as required by station procedures. Specifically, personnel did not generate the required

condition reports and adequately document the investigations for six instances of

unplanned or un-briefed electronic dosimeter alarms that occurred between January

2009 and March 2009. The performance deficiency resulted in workers receiving

unanticipated dose rate alarms with no formally-documented investigation prior to

returning to work in a Radiologically Controlled Area. Entergy entered the finding into

the corrective action program as condition report CR-IP3-2009-01253 and 01318.

The finding is more than minor because it is associated with the Occupational Radiation

Safety cornerstone attribute of programs and process, and adversely affected the

objective to ensure adequate protection of worker health and safety from exposure to

radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and

implement programs to keep exposures as low as reasonably achievable, because

7

Enclosure

multiple examples were identified regarding the failure to satisfy station radiation

protection procedures. Using the Occupational Radiation Safety Significance

Determination Process, the inspectors determined that the finding was of very low safety

significance (Green) because it did not involve: (1) as low as is reasonably achievable

planning and controls, (2) an overexposure of an individual, (3) a substantial potential for

overexposure, or (4) an impaired ability to assess dose.

The inspectors determined that the finding had a cross-cutting aspect related to

procedural adherence in the work practices component of the human performance area.

Specifically, Entergy personnel did not follow procedures to generate condition reports

and document investigations when high dose-rate alarms were received by workers.

H.4(b) per IMC 0305] (Section 2OS1)

B.

Licensee-Identified Violations

None.

8

Enclosure

REPORT DETAILS

Summary of Plant Status

Indian Point Nuclear Generating (Indian Point) Unit 2 began the inspection period at full reactor

power and remained at or near full power during the quarter.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 1 sample)

Impending Adverse Weather

a.

Inspection Scope

The inspectors reviewed the overall preparations and protection of risk-significant

systems for extremely cold weather conditions from January 14 - 19, 2009. The

inspectors reviewed and assessed implementation of the sites adverse weather

preparation procedures and compensatory measures for the affected conditions before

the onset of and during the cold weather conditions. This included verification that

operator actions defined in their adverse weather procedure maintain readiness of

essential systems that are vulnerable to freezing temperatures. The inspectors verified

Entergy personnel implemented periodic equipment walkdowns or other measures to

ensure the condition of plant equipment was operable.

The inspectors also reviewed Entergys corrective action program to review previous

issues associated with cold weather preparations and freezing conditions. Documents

reviewed are listed in the attachment.

b.

Findings

Introduction. The inspectors identified a Green finding because Entergy personnel did

not adequately implement procedure EN-LI-102, Corrective Action Process, and

promptly identify a condition adverse to quality associated with stuck-open louvers in a

fire protection pump room following pump testing on January 14, 2009.

Description. On January 17, 2009, during a period of sustained cold weather which

included sub-zero temperatures, control room personnel received a fire panel trouble

alarm indicative of a low-pressure condition in the fire header and dispatched a plant

operator to investigate. The operator identified spraying water from the body of a

ruptured six-inch fire protection valve located in the 11 fire pump house. The operator

isolated the broken valve from the fire header by shutting a manually-operated upstream

valve which stopped the water spray. In addition, the operator observed that the pump

house room was significantly colder than expected and subsequently identified the

rooms ventilation louvers to the outside were mechanically bound in the open position.

The operator disconnected the louver linkage and manually shut the louvers.

9

Enclosure

On January 21, 2009, the inspectors identified a second six inch valve that was cracked

due to the previous cold weather (freezing) conditions in the fire pump house. Entergy

personnel entered this issue into the corrective action program and performed site

walkdowns to identify additional adverse conditions associated with the cold weather.

The inspectors determined that Entergy did not fully implement Entergy procedure EN-

LI-102, Corrective Action Process. Specifically, EN-LI-102 requires plant personnel to

identify adverse conditions, including cold-weather related conditions, and then enter

them into the CAP for resolution. Attachment 9.2 of the procedure provides examples of

adverse conditions expected to be reported; Section 1 of the Attachment contains

examples of operational conditions requiring entry into the CAP including "events or

conditions that could negatively impact reliability or availability." Additionally, plant

operators should have had heightened awareness to cold weather conditions because

Entergy procedure OAP-008, "Severe Weather Preparations," requires in step 4.3.7,

when freezing conditions are expected, that increased monitoring of plant areas to

monitor for adverse effects on plant equipment and verify that adequate protection is

provided. Operations personnel did not identify abnormal conditions in the 11 fire pump

room that led to the freezing and subsequent rupture of fire protection components.

The inspectors determined it was reasonable for Entergy personnel to identify this issue

because operators should have identified that the louvers failed to shut following a

routine operations test of 11 fire pump on January 14, 2009. In addition, operators

perform tours of the pump house every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and should have identified the room

was much colder than normal.

Analysis. The inspectors identified a performance deficiency because Entergy

personnel did not implement procedure guidance and identify stuck open louvers and a

subsequent second cracked fire header valve in the 11 fire pump house. The finding

was more than minor because it was associated with the protection against external

factors attribute of the Mitigating Systems cornerstone and it affected the cornerstone

objective of ensuring the reliability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the failure of the six-inch valves impacted the

reliability of the fire header until the ruptured valve was isolated.

This finding was evaluated using Phase 1 of Inspection Manual Chapter (IMC) 0609

Appendix F, Fire Protection Significance Determination Process. The inspectors

determined the issue was of very low safety significance (Green) because the cracked

fire valves were easily isolated and did not pass sufficient water to render the fire

header non-functional. Specifically, the inspectors assigned a low degradation rating to

the fire header because the fire pumps were able to maintain pressure in the fire header

until the ruptured valves were isolated.

The inspectors determined that the finding had a cross-cutting aspect in the area of

human performance related to work practices - human error prevention techniques.

Specifically, Entergy personnel routinely tour the 11 fire pump house did not question

the abnormally cold room temperatures. (H.4(a) per IMC 0305)

Enforcement: Enforcement action does not apply because the performance deficiency

did not involve a violation of a regulatory requirement. Because this finding does not

involve a violation of regulatory requirements and has very low safety significance, it is

identified as FIN 05000247/2009002-01, Failure to Identify Open Louvers in 11 Fire

Pump House.

10

Enclosure

1R04 Equipment Alignment (71111.04Q - 3 samples)

Partial System Walkdowns

a.

Inspection Scope

The inspectors performed partial system walkdowns to verify the operability of redundant

or diverse trains and components during periods of system train unavailability, or

following periods of maintenance. The inspectors referenced the system procedures,

the UFSAR, and system drawings to verify the alignment of the available train supported

its required safety functions. The inspectors also reviewed applicable condition reports

(CR) and work orders to ensure Entergy personnel identified and properly addressed

equipment discrepancies that could potentially impair the capability of the available train,

as required by Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix

B, Criterion XVI, Corrective Action. The documents reviewed during these inspections

are listed in the Attachment.

The inspectors performed a partial walkdown on the following systems, which

represented three inspection samples:

21 and 22 component cooling water (CCW) system train when 23 CCW pump

was tagged out for maintenance;

City water system as a supply to auxiliary boiler feedwater (ABFW) when the

condensate storage tank was declared inoperable due to leakage;

21 and 23 ABFW trains when 22 ABFW pump was tagged out and temporary

modifications were applied to 21 and 23 ABFW minimum flow lines.

b.

Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05Q - 5 samples)

a.

Inspection Scope

The inspectors conducted tours of several fire areas to assess the material condition and

operational status of fire protection features. The inspectors verified, consistent with the

applicable administrative procedures, that: combustibles and ignition sources were

adequately controlled; passive fire barriers, manual fire-fighting equipment, and

suppression and detection equipment were appropriately maintained; and compensatory

measures for out-of-service, degraded, or inoperable fire protection equipment were

implemented in accordance with Entergys fire protection program. The inspectors

evaluated the fire protection program for conformance with the requirements of License

Condition 2.K. The documents reviewed during this inspection are listed in the

Attachment. This inspection represented five inspection samples for fire protection

tours, and was conducted in the following areas:

FZ 65, Main Steam/Feed Regulating Valve Areas;

FZ 23, 62A Auxiliary Feed Pump Room & Building;

FZ 14, 480V Vital AC Switchgear Room;

FZ 10, Emergency Diesel Generator Building; and

FZ 360, Station Blackout Diesel Area.

11

Enclosure

b.

Findings

.1

Failure to Identify Damaged Components in EDG Ventilation Motor Control Center

Introduction: The inspectors identified a NCV of very low safety significance (Green)

related to 10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, because Entergy

personnel did not promptly identify and correct an adverse condition related to an

electrical fault. Specifically, personnel did not identify a safety-related cubicle (bucket)

had experienced a fault prior to replacement of upstream fuses and restoration of power

to the cubicle.

Description: On January 28, 2009, operations personnel detected an acrid odor coming

from the emergency diesel generator (EDG) building. Operators entered the EDG

building to investigate the source of the acrid odor and identified that a MCC was de-

energized. Operations personnel did not identify external damage to the MCC; however,

operators did not open MCC panels to inspect for internal damage. Operators checked

the upstream 175 amp supply fuses, located in a different building, and identified that 2

of 3 fuses had blown. Operators opened the downstream breakers on the MCC in the

EDG building and then replaced the 175 amp supply fuses in the control building. Once

operators replaced the blown fuses, they re-energized the EDG building MCC#1, and

subsequently began to locally shut all of the cubicle switches. When operators

attempted to shut the switch associated with cubicle 4N, the switch did not function as

expected. Operators then opened the panel for cubicle 4N and identified charred

electrical components.

Entergy personnel generated a D level condition report (CR) for cubicle 4N on the

basis that it supplies a non safety-related (NSR) EDG room heater. Entergy personnel

closed the CR to a work request to troubleshoot and repair the NSR heater. However,

the inspectors questioned the classification of the MCC and determined that the charred

components were safety related (SR). Cubicle 4N contains a SR main line switch and

SR 30 amp main line fuses. The 30 amp fuses are SR to isolate the NSR heaters from

the MCC in the event of a room heater fault. The inspectors also questioned the

appropriateness of leaving the damaged cubicle in the energized MCC. Following

inspector questions, Entergy staff issued another CR and removed the damaged cubicle

from the MCC on February 11. During removal of the charred cubicle, maintenance

personnel were unable to disconnect the main line cables due to arc-welding at the

termination and subsequently had to cut two of the three cables upstream of the

termination and cubicle switch. These cables and the line side of the switch were

energized from January 28 until February 11. After the damaged cubicle was removed,

engineering personnel performed an inspection and determined that the fault originated

from a high resistance connection on the C phase between the main fuse clip and the

cubicle supply switch in the 4N cubicle.

The inspectors determined that replacing the upstream 175 Amp fuses on and restoring

power to the EDG ventilation MCC #1, which contained the charred 4N cubicle, without

identifying the source of the acrid odor could have reinitiated the fault and increased the

probability of a fire. In addition, operations personnel tried to locally close the damaged

switch which could have also re-initiated the fault. Entergy staff also did not take action

to remove or de-energize the charred cubicle after the condition was identified on

January 28, 2009. The damaged cubicle was de-energized and removed from the MCC

on February 11 in response to the inspectors questions.

12

Enclosure

This issue was reasonable for the licensee to foresee and correct because acrid odor is

an indication of a fault. It was reasonable for Entergy personnel to open panel doors

and perform visual inspections of the affected MCC prior to replacing upstream fuses

and restoring power to the fault. The inspectors determined that the National Electrical

Code NFPA 70E, Standard for Electrical Safety in the Workplace, prohibits

reenergizing a circuit after a protective device has operated until it has been determined

that the automatic operation was a result of an overload and not a fault. The acrid odor

in the EDG building was an indication of a fault vice an overload condition. In addition,

once Entergy personnel identified the cubicle was charred and experienced an electrical

fault, industry standards would have operators immediately secure power and/or

remove the damaged gear from the MCC.

Entergy entered the issue into the corrective action program as IP2-2009-00342 and

IP2-2009-00483, trained all operations personnel on the requirements to replace fuses

and re-energize electrical equipment, and plans to review operations procedures for

operating electrical equipment.

Analysis: The inspectors determined that Entergys failure to promptly identify an

adverse condition associated with damaged electrical components constituted a

performance deficiency. This issue was more than minor because the finding was

associated with the external factors attribute of the Initiating Events cornerstone and

impacted the cornerstone objective of limiting the likelihood of those events that upset

plant stability and challenge critical safety systems during shutdown as well as power

operations. Specifically, operations personnel did not identify the source of the acrid

odor, indicative of an electrical fault, in the EDG building; re-energized damaged

electrical equipment; and left damaged electrical components (cubicle 4N) energized for

14 days prior to its removal from the MCC. The inspectors determined these issues

increased the likelihood of a fire in the EDG building. The condition was evaluated by a

Senior Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire Protection

Significance Determination Process. It was determined that in the event of a fire

consuming the MCC, no transient would be placed on the plant and no components

required to safely shutdown the plant would be impacted. As a result, in accordance

with task 2.3.5 of Appendix F, the issue was screened to Green.

The inspectors determined that a cross-cutting aspect was associated with this finding

in the area of human performance related to conservative decision making. Specifically,

Entergys decision-making was non-conservative as it related to the processes used to

identify the source of the acrid odor; re-energize the damaged electrical equipment; and

keep a damaged electrical component energized for 14 days prior to its removal from

the MCC. (H.1(b) per IMC 0305)

Enforcement: 10 CFR 50 Appendix B, Criterion XVI, Corrective Action, requires that

measures shall be established to assure conditions adverse to quality, such as failures

and malfunctions are promptly identified and corrected. Contrary to the above, on

January 28, 2009, operations personnel did not identify that a safety-related bucket had

experienced a fault prior to replacing upstream fuses and restoring power to the bucket.

In addition, after replacing the upstream fuses, operations personnel tried to locally shut

the damaged cubicle switch and left damaged equipment energized until February 11,

2009. Entergy entered the issue into the corrective action program as IP2-2009-00342

and IP2-2009-00483, trained all operations personnel on the requirements to replace

fuses and re-energize electrical equipment, and plans to review operations procedures

13

Enclosure

for operating electrical equipment. Because the violation was of very low safety

significance and it was entered into the licensees corrective action program, this

violation is being treated as an NCV, consistent with the NRC Enforcement Policy: NCV 05000247/2009002-02, Failure to Identify Damaged Components in EDG

Ventilation Motor Control Center.

.2

Degraded Fire Door to the 480V Vital Bus Room

Introduction: The inspectors identified a NCV of very low safety significance (Green)

related to License Condition 2.K., fire protection program, because Entergy personnel

did not promptly identify and correct a degraded three-hour rated fire door on the west

entrance of the 480 Volt switchgear room.

Description: License Condition 2.K., fire protection program, requires that Entergy

implement and maintain in effect all provisions of the NRC-approved fire protection

program, as approved in part by the NRC Safety Evaluation Report (SER) dated

January 31, 1979. The January 31, 1979, SER requires administrative controls

comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for

Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch

Technical Position (BTP) 9.5-1 requires that measures be established to assure that

conditions adverse to fire protection, such as deficiencies, deviations, defective

components, and non-conformities are promptly identified, reported, and corrected.

On February 6, 2009, the inspectors performed a fire protection walkdown of the 480-

Volt switchgear room. The inspectors noted the three-hour rated, swing-type fire door

on the west side of the 480-Volt switchgear room was not latched closed. The

inspectors observed the door being held open by the latch mechanism which had not

repositioned to allow the door to shut. The inspectors observed the latch mechanism

did not move freely preventing the door from shutting automatically. The inspectors

shut the door and notified shift operations personnel who tightened latch screws on the

door and wrote a condition report.

On February 18, the inspectors identified the 480-Volt switchgear room door was not

latched shut again. The inspectors determined the door could not be closed due to

interference from the latch mechanism screw which had backed out. The inspectors

notified operations of the fire door issue. Operations personnel re-inserted the latch

mechanism screw and documented the issue in a condition report. The inspectors

questioned whether it was appropriate to re-insert a screw that had backed out on its

own in such a short period of time. Entergy personnel subsequently inspected the door

on February 23 and identified the screws holding the latch mechanism to the door were

stripped. Entergy personnel tapped new holes in the door latch mechanism and

installed new screws.

On March 3, inspectors identified the 480-Volt switchgear room fire door not latched

shut again. The inspectors observed the door was being held open by the latch

mechanism which had not repositioned to allow the door to shut. The inspectors noted

the latch mechanism did not move freely preventing the door from shutting

automatically. The inspectors notified operations personnel of the non-functioning fire

door and Entergy subsequently had a locksmith inspect the latch. The locksmith

installed a new latch mechanism on March 3 and determined the latch issues observed

were age-related due to interaction of wear products from the latch interfering with the

moving portions of the latch, as a result of latching and unlatching door operations.

14

Enclosure

Entergy entered the issue into the corrective action program on March 3, performed an

inspection of all fire doors onsite, and identified and corrected issues with other required

fire doors.

Analysis: The inspectors identified a performance deficiency because Entergy personnel

did not identify and correct the non-functional fire door. The finding was more than

minor because it is associated with the protection against external factors attribute of

the Mitigating Systems cornerstone and affected the cornerstone objective of ensuring

the reliability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, in the event of a large fire in the 480-Volt switchgear room

or the turbine building, the affected fire door is credited to prevent the spread of fire from

one area to the other area. This fire door, when degraded, impacts the reliability of

mitigating systems in the 480-Volt switchgear room that are relied upon during a large

fire in the turbine building, and vice versa.

This finding was evaluated using Phase 1 of IMC 0609 Appendix F, Fire Protection

Significance Determination Process. Since the area in question had a fire watch

posted during the time the door was degraded, an adequate level of protection was

maintained to compensate for the degraded door and resulted in the finding being of

very low safety significance. As such according to task 1.3.1, the inspectors determined

the finding was Green.

The inspectors determined that the finding had a cross-cutting aspect in the area of

problem identification and resolution because Entergy personnel did not thoroughly

evaluate a degraded fire door latch on several occasions, such that the resolution of the

problems addressed the causes. (P.1(c) per IMC 0305)

Enforcement: License Condition 2.K., fire protection program, requires that Entergy

implement and maintain in effect all provisions of the NRC-approved fire protection

program, as approved in part by the NRC Safety Evaluation Report (SER) dated

January 31, 1979. The January 31, 1979, SER requires administrative controls

comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for

Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch

Technical Position 9.5-1 requires that measures be established to assure that conditions

adverse to fire protection, such as deficiencies, deviations, defective components, and

non-conformities are promptly identified, reported, and corrected.

Contrary to the above, Entergy personnel did not promptly identify and then

subsequently correct the non-functional 480-Volt switchgear fire door. This fire door

was identified by inspectors in a non-functional state on February 6, February 18, and

again on March 3, 2009. Entergy entered the issue into the corrective action program

as IP2-2009-00526, IP2-2009-00680, IP2-2009-00709, IP2-2009-00834, IP2-2009-

00842, and IP2-2009-00843. Because the violation was of very low safety significance

and it was entered into the licensees corrective action program, this violation is being

treated as an NCV, consistent with the NRC Enforcement Policy: NCV 05000247/2009002-03, Failure to Identify and Promptly Correct Degraded 480-Volt

Switchgear Room Fire Door.

1R07 Heat Sink Performance (71111.07A - 1 sample)

a.

Inspection Scope

15

Enclosure

The inspectors selected the 22 component water heat exchanger for review to

determine the heat exchangers readiness and availability to perform its safety functions.

The inspectors reviewed the design basis for the component, reviewed Entergy

commitments to NRC Generic Letter 89-13, and reviewed engineering reports that

documented results of previous internal inspections. The inspectors also observed the

disassembly, inspection, and cleaning of the heat exchanger and reviewed engineering

results of the inspection to verify that appropriate corrective actions were initiated for

deficiencies that were discovered. The inspectors reviewed documents for and verified

that the amount of tubes plugged within the heat exchanger did not exceed the

maximum amount allowed. Documents reviewed are listed in the appendix.

b.

Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

Quarterly Review (71111.11Q - 1 sample)

a.

Inspection Scope

On February 23, 2009, the inspectors observed licensed operator simulator training

associated with a sustained loss of all alternating current (AC) power scenario, to verify

that operator performance was adequate, and that evaluators were identifying and

documenting crew performance problems. The inspectors evaluated the performance of

risk-significant operator actions, including the use of emergency operating procedures.

The inspectors assessed the clarity and effectiveness of communications, the

implementation of appropriate actions in response to alarms, the performance of timely

control board operation and manipulation, and the oversight and direction provided by

the control room supervisor. The inspectors also reviewed simulator fidelity with respect

to the actual plant. The inspectors evaluated licensed operator training for conformance

with the requirements of 10 CFR Part 55, Operator Licenses. The documents

reviewed during this inspection are listed in the Attachment. This observation of

operator simulator training represented one inspection sample.

b.

Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12Q - 3 samples)

a.

Inspection Scope

The inspectors reviewed performance-based problems that involved structures,

systems, and components (SSCs) to assess the effectiveness of maintenance activities.

When applicable, the reviews focused on:

Proper Maintenance Rule scoping in accordance with 10 CFR 50.65;

Characterization of reliability issues;

Changing system and component unavailability;

16

Enclosure

10 CFR 50.65(a)(1) and (a)(2) classifications;

Identifying and addressing common cause failures;

Trending of system flow and temperature values;

Appropriateness of performance criteria for SSCs classified (a)(2); and

Adequacy of goals and corrective actions for SSCs classified (a)(1).

The inspectors also reviewed system health reports, maintenance backlogs, and

Maintenance Rule basis documents. The inspectors evaluated maintenance

effectiveness and monitoring activities against the requirements of 10 CFR 50.65. The

documents reviewed during this inspection are listed in the Attachment. The following

Maintenance Rule samples were reviewed and represented three inspection samples:

RWST level indication system;

EDG fuel injection system; and

480-Volt switchgear system.

b.

Findings

Introduction: The inspectors identified a NCV of very low safety significance (Green)

related to TS 5.4.1, Administrative Controls: Procedures, because Entergy did not

maintain an adequate maintenance procedure for a safety-related electrical motor

control center (MCC). Specifically, the eight-year maintenance procedure for the

affected EDG ventilation MCC did not contain an adequate method to identify high

resistance connections within the cubicle.

Description: On January 28, 2009, operations personnel identified an acrid odor coming

from the EDG building. Subsequent personnel investigation revealed a charred cubicle

in a safety-related 480-Volt MCC. Specifically, cubicle 4N, in the EDG ventilation MCC,

experienced a phase-to-phase fault that caused the upstream 175 amp fuses to open

and de-energize the MCC. Entergy personnel subsequently generated a condition

report (CR) that was closed to a work request to troubleshoot and repair the cubicle.

Entergy personnel removed the damaged cubicle from the MCC on February 6 and

determined the likely cause to be a high-resistance connection between the cubicle

switch and 30 amp fuse clip on the C phase resulting in long-term overheating. This

overheating condition degraded the insulation between two of the three phases over

time and eventually resulted in a phase-to-phase fault on January 28, 2009.

The inspectors reviewed the 8-year maintenance procedure 2-MCC-003-ELC,

Klockner-Moeller, Series 200, 480 Volt Motor Control Center Preventive Maintenance,

which was performed on the affected EDG ventilation MCC on April 6, 2008. The

inspectors noted that the procedure was revised the same day to allow performance of

the maintenance without de-energizing the equipment. The revision resulted in portions

of the cubicle cleaning and inspection procedure not being performed because they

could not be safely performed while the cubicle was energized. The inspectors

determined that the procedure revision on April 6, 2008, was inappropriately treated as

an editorial revision without a technical evaluation of the change performed. In addition,

following interviews with Entergy personnel, it was determined that maintenance had not

been performed on this MCC prior to April 6, 2008.

17

Enclosure

The inspectors reviewed industry guidance for performing switchgear maintenance and

determined that Entergy did not include standard maintenance practices typically

utilized by its staff that would have identified a high resistance connection in the cubicle.

Specifically, continuity checks across contacts and switches were not performed, fuse

clip tensions and tightness were not performed, and all terminations could not be

checked due to the decision to perform the maintenance with portions of the cubicle

energized. In addition, the inspectors determined the EDG ventilation MCCs were not

included in Entergys thermography program, contrary to Entergy corporate preventive

maintenance templates. The inspectors determined that not performing thermography

on the EDG ventilation MCC constituted a missed opportunity to identify the high

resistance condition.

It is reasonable to consider the high resistance connection existed during the

maintenance performed on April 6, 2008, because high resistance connections do not

develop into phase-to-phase faults over a short period of time. This is an underlying

assumption for performing switchgear maintenance, which is intended to identify and

correct loose/high resistance connections, on an eight-year periodicity. In addition,

Entergys corporate template for switchgear maintenance recommends a six-year

periodicity and thermography every year. It is reasonable to expect Entergy to be aware

of the existing industry guidance as well as the Entergy corporate maintenance

templates.

Entergy entered the issue into the CAP as IP2-2009-00342 and IP2-2009-00483,

scoped the EDG ventilation MCC into the existing thermography program, performed an

extent-of-condition review that identified 21 additional panels that should be in the

thermography program, and plans to revise the maintenance procedure.

Analysis: The inspectors identified a performance deficiency because Entergy did not

maintain an adequate maintenance procedure for the safety-related EDG ventilation

MCC. This issue was more than minor because the finding was associated with the

external factors attribute of the Initiating Events cornerstone and impacted the initiating

events cornerstone objective of limiting the likelihood of those events that upset plant

stability and challenge critical safety systems during shutdown as well as power

operations. Specifically, the high resistance connection degraded into a phase-to-phase

fault and increased the likelihood of a fire in the EDG building. The condition was

evaluated by a Senior Reactor Analyst utilizing Phase 2 of IMC 0609 Appendix F, Fire

Protection Significance Determination Process. It was determined that in the event of a

fire consuming the MCC, no transient would be placed on the plant and no components

required to safely shutdown the plant would be impacted. As a result, in accordance

with task 2.3.5 of Appendix F, the issue was screened to Green.

The inspectors determined that the finding had a cross-cutting aspect associated with

the area of problem identification and resolution related to the use of operating

experience (OE). Specifically, Entergy personnel did not implement industry

recommended practices, or an alternate equivalent method, for identifying high

resistance connections in electrical switchgear. (P.2(b) per IMC 0305)

Enforcement. TS 5.4.1 Administrative Controls: Procedures, states, Written

procedures shall be established, implemented, and maintained covering the

requirements and recommendations of Appendix A of Regulatory Guide (RG) 1.33,

Revision 2. Appendix A of RG 1.33 requires procedures for maintenance activities that

18

Enclosure

can affect the performance of safety related equipment. Contrary to the above, Entergy

did not maintain a maintenance procedure for a safety-related MCC cubicle.

Specifically, the eight-year maintenance procedure, first performed on April 6, 2008, did

not contain an adequate method to identify and correct high resistance connections in

the cubicle. Entergy entered the issue into the CAP as IP2-2009-00342 and IP2-2009-

00483. Because the violation was of very low safety significance and it was entered into

the licensees corrective action program, this violation is being treated as an NCV,

consistent with the NRC Enforcement Policy: NCV 05000247/2009002-04, Inadequate

Maintenance Procedure for EDG Ventilation Motor Control Center.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 6 samples)

a.

Inspection Scope

The inspectors reviewed scheduled and emergent maintenance activities to verify the

appropriate risk assessments were performed prior to removing equipment from service

for maintenance or repair. The inspectors verified that risk assessments were performed

as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent

work was performed, the inspectors verified the plant risk was promptly reassessed and

managed. Documents reviewed during this inspection are listed in the Attachment. The

following activities represented six inspection samples:

Emergent maintenance on the 22 EDG lube oil pump during the 23 EDG

maintenance outage;

Planned risk during 21 auxiliary boiler feedwater (ABFW) pump outage and reactor

protection system testing;

Unplanned elevated risk condition due to delayed work on reactor protection system

components during planned maintenance of 22 ABFW pump;

Planned maintenance on a reactor water storage tank level indicator;

Planned maintenance on the 22 ABFW pump while temporary modifications were

applied to the 21 and 23 ABFW pumps; and

Planned risk during 23 EDG testing and maintenance.

b.

Findings

Introduction: The inspectors identified a NCV of very low safety significance (Green)

related to 10 CFR 50.65(a)(4) because Entergy staff did not adequately assess the risk

associated with the unavailability of the Refueling Water Storage Tank (RWST) level

indication during planned maintenance on the level transmitters and instrumentation.

Description: On February 6, 2009, Entergy staff performed maintenance on the RWST

level indication system. The inspectors identified that the online risk assessment did not

consider planned maintenance on the RWST level indication, as required by 10 CFR

50.65(a)(4). The inspectors reviewed the work activity and noted the maintenance

scheduling software used by Entergy did not have the RWST maintenance coded as a

risk-significant activity. Entergys maintenance planning process prompts the

organization to evaluate the risk impact of all maintenance activities coded as risk-

significant. Therefore, a risk assessment was not performed for the quarterly RWST

level indication maintenance as required. In addition, the RWST level indication was not

represented in Entergys interactive risk model. Entergy staff subsequently updated the

risk model to include the RWST level indication and subsequently assessed the online

19

Enclosure

risk for the maintenance which resulted in a measurable increase in the core damage

frequency (CDF). The increase in CDF was not large enough to require entrance into

the higher risk category per Entergy procedures. In addition, the increase in CDF (1.1E-

6) combined with the limited duration of the maintenance (15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />) resulted in a

relatively small incremental core damage probability deficit (1.9E-9).

The inspectors determined this same maintenance activity is modeled in the Indian Point

Unit 3 risk model. Entergy entered the issue into the corrective action program (CR-IP2-

2009-00342), updated the risk model to include the maintenance activity, assessed the

risk, and appropriately coded the maintenance activity to ensure it would be risk

assessed in the future.

Analysis: The inspectors identified a performance deficiency in that Entergy staff did not

assess the increase in plant risk resulting from planned maintenance activities on RWST

level instrumentation as required by 10 CFR 50.65(a)(4). The inspectors determined

that this finding was more than minor because it was a risk assessment issue in which

Entergy personnel did not consider risk significant SSCs that were unavailable during

maintenance. Specifically, RWST level indication is included in Table 2 of the plant

specific Phase 2 SDP risk-informed inspection notebook. The inspectors assessed the

significance of this issue in accordance with IMC 0609, Appendix K, Maintenance Risk

Assessment and Risk Management Significance Determination Process. The

inspectors determined that this finding was of very low safety significance (Green)

because the incremental core damage probability deficit was less than 1E-6.

The inspectors determined that the finding had a cross-cutting aspect in human

performance related work control. Specifically, Entergy personnel did not appropriately

plan work activities by incorporating risk insights for affected plant equipment. (H.3(a)

per IMC 0305)

Enforcement: 10 CFR 50.65 (a)(4) states, in part that licensees shall assess and

manage the increase in risk that may result from the proposed maintenance activities

before performing those activities. Contrary to the above, on February 6, 2009, Entergy

performed maintenance on the RWST level indication system without assessing the

increase in risk. Entergy entered the issue into the corrective action program (CR-IP2-

2009-00342. Because this issue is of very low safety significance and is entered into

Entergys corrective action program, this violation is being treated as an NCV consistent

the NRC Enforcement Policy: NCV 05000247/2009002-05, Failure to Include RWST

Level Maintenance In Online Risk Assessment.

1R15 Operability Evaluations (71111.15 - 7 samples)

a.

Inspection Scope

The inspectors reviewed operability evaluations to assess the acceptability of the

evaluations, the use and control of compensatory measures when applicable, and

compliance with Technical Specifications. The inspectors reviews included verification

that operability determinations were performed in accordance with procedure

ENN-OP-104, Operability Determinations. The inspectors assessed the technical

adequacy of the evaluations to ensure consistency with the Technical Specifications,

UFSAR, and associated design basis documents. The documents reviewed are listed in

20

Enclosure

the Attachment. The following operability evaluations were reviewed and represented

seven inspection samples:

Proximity of 480-Volt vital motor control center to an uninsulated steam line;

Leakage from condensate storage tank (CST) return piping;

Impacts of scaffolding built in the vicinity of the 21 and 22 component cooling water

heat exchangers;

Impact on pressurizer surge line and reactor coolant system piping while performing

reactor plant startups and shutdowns due to thermal transients;

Performance impact on the 21 and 22 auxiliary component cooling pumps (ACCPs)

with respect to a potential hydraulic lock-out condition of the 21 ACCP due to 22

ACCP larger impeller size;

Mechanical failure of a grease fitting on 21 service water pump; and

Low temperatures in condensate storage tank volume.

b.

Findings

No findings of significance were identified. With respect to the CST return piping, the

inspectors determined Entergy operators maintained the CST aligned to supply water to

the AFW pumps. The inspectors concluded the leakage did not prevent the CST from

fulfilling its safety function. Specifically, design features of the CST and the elevation of

the return line relative to the leak location provided assurance that, in the event the CST

return line leak increased significantly, the CST water volume would have been

maintained above TS minimum required water level and able to supply the required

water to the auxiliary feedwater system.

1R18 Plant Modifications (71111.18 - 2 samples)

.1

Temporary Modifications

a.

Inspection Scope

The inspectors reviewed one temporary plant modification package for securing

minimum flow lines on the motor driven auxiliary boiler feedwater pumps (ABFPs) and

controlling the operation on the ABFPs through a temporary operating procedure during

repairs of the CST return piping. The inspectors verified the design bases, licensing

bases, and performance capability of the system was not degraded by the temporary

modification. The inspectors review included Entergys engineering evaluation for

determining the ABFPs could start with the pumps required minimum flow being

achieved through the internal thrust balance lines while the minimum flow lines were

isolated. In addition, the inspectors interviewed plant staff, and reviewed issues entered

into the corrective action program to determine whether Entergy had been effective in

identifying and resolving problems associated with the temporary modification. The

documents reviewed are listed in the Attachment.

b.

Findings

No findings of significance were identified.

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Enclosure

.2

Permanent Modifications

a.

Inspection Scope

The inspectors reviewed modification documents associated with the installation of an

additional nitrogen backup power supply for the 21- 24 steam generator atmospheric

dump valves. The inspector verified that the modification was reviewed adequately to

verify the modification conformed to design criteria and did not interfere or invalidate

previous design assumptions or functions. The documents reviewed are listed in the

Attachment.

b.

Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19 - 6 samples)

a.

Inspection Scope

The inspectors reviewed post-maintenance test procedures and associated testing

activities for selected risk-significant mitigating systems, and assessed whether the

effect of maintenance on plant systems was adequately addressed by control room and

engineering personnel. The inspectors verified that: test acceptance criteria were clear,

the test demonstrated operational readiness and were consistent with design basis

documentation; test instrumentation had current calibrations, and appropriate range and

accuracy for the application; and the tests were performed as written, with applicable

prerequisites satisfied. Upon completion of the tests, the inspectors verified that

equipment was returned to the proper alignment necessary to perform its safety function.

Post-maintenance testing was evaluated for conformance with the requirements of 10

CFR 50, Appendix B, Criterion XI, Test Control. The documents reviewed are listed in

the Attachment. The following post-maintenance activities were reviewed and

represented six inspection samples:

Replacement of SG 23 pressure indicator PI-1355;

22 component cooling water heat exchanger following maintenance;

21 charging pump following recirculation valve maintenance;

Condensate storage tank return line following pipe section replacement;

Emergency diesel generator air compressor following quarterly maintenance; and

23 emergency diesel generator following quarterly engine maintenance.

b.

Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22 - 6 samples)

a.

Inspection Scope

The inspectors observed performance of portions of surveillance tests and/or reviewed

test data for selected risk-significant SSCs to assess whether they satisfied Technical

Specifications, UFSAR, Technical Requirements Manual, and Entergy procedure

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Enclosure

requirements. The inspectors verified that: test acceptance criteria were identified,

demonstrated operational readiness, and were consistent with design basis

documentation; test instrumentation had accurate calibration, and appropriate range and

accuracy for the application; and tests were performed as written, with applicable

prerequisites satisfied. Following the tests, the inspectors verified that the equipment

was capable of performing the required safety functions. The inspectors evaluated the

surveillance tests against the requirements in Technical Specifications. The documents

reviewed during this inspection are listed in the Attachment. The following surveillance

tests were reviewed and represented six inspection samples:

2-PT-Q031A, 21 Auxiliary Component Cooling Pump In-Service Test;

2-PT-Q054, Pressurizer Level Bistables;

2-PT-Q013 DS027, IST Valve Test of 888A (Safety Injection Pump Suction from

Residual Heat Removal heat Exchanger);

2-PT-2M4, Safety Injection System Train A Actuation Logic and Master Relay Test;

2-PT-Q030C, 23 Component Cooling Water Pump; and

0-SOP-LEAKRATE-001, RCS Leakrate Surveillance, Evaluation, and Leak

Identification.

b.

Findings

Introduction. The inspectors identified a NCV of very low safety significance (Green)

related to 10 CFR 50.55a, Codes and standards, because Entergys procedure 2-PT-

Q031A did not contain appropriate acceptance criteria for determining that safety-

related check valves performed their safety function when required in accordance with

the American Society of Mechanical Engineers (ASME) OM Code.

Description. Entergy procedure 2-PT-Q031A, 21 Auxiliary Component Cooling Pump

(ACCP), is an In-Service Test (IST) procedure that demonstrates the operability of the

21 ACCP, the pump bypass line check valve (755), the 21 ACCP discharge check valve

(755B), and the 22 ACCP discharge check valve (755A) in accordance with Technical

Specification (TS) 5.5.6, Inservice Testing Program.

The test established a single acceptance criterion to determine if the discharge check

valve on the 22 ACCP train shuts when the parallel trains 21 ACCP is providing design

flow. The acceptance criterion was that no reverse rotation is observed on the 22

ACCP. Although NUREG-1482, Guidelines for Inservice Testing at Nuclear Power

Plants identifies the methodology of using reverse pump rotation as an acceptable

means of testing, Entergys site-specific experience in 2005 demonstrated this particular

method was not effective to maintain the ACCP discharge check valve safety function.

Specifically, when 2-PT-Q031A was performed on January 19, 2005, the 21 ACCP

failed the performance test because check valve 755A was determined to be in the

open position. However, the 22 ACCP did not rotate in the reverse direction. Following

disassembly of valve 755A, engineers determined the valve remained in the open

position because of excessive clearances between the hinge pin and hinge pin

bushings. Entergy personnel determined the check valve was likely in this condition

following maintenance on the valve in late 2004. CR-IP2-2005-0252 was written to

document and evaluate the issue. The issue was previously documented in LER 05000247/2005001-00 and NRC NCV 50-247/2005003-01. At that time, Entergy

personnel concluded the test criteria established in 2-PT-Q031A was acceptable but

that post-maintenance tests on the check valve should include amplifying comments

23

Enclosure

directing the performance of the IST following maintenance. Entergy personnel

concluded that the IST was adequate because the low pump head that caused the

pump performance test to fail led to troubleshooting that identified that check valve

755A was stuck open.

The inspectors determined that the criterion for determining operability of 755A in test 2-

PT-Q013A was inadequate because the criterion in the procedure previously failed to

identify that 755A remained in the open position in January 2005 and 2-PT-Q013A does

not identify any other criteria, including using pump head, to determine operability of

755A. Additionally, the inspectors determined the test criterion for check valve 755A

and 755B were not consistent with the following ASME Code requirements:

The ASME OM Code 2001 Subsection ISTA-3160 states that procedures shall

contain the Owner-specified reference values and acceptance criteria;

The ASME OM Code 2001 Subsection ISTC-1400 (c) states it is the Owners

responsibility to ensure that the application, method, and capability of each

nonintrusive technique is qualified; and

The ASME OM Code 2001 Subsection ISTC-3530 states obturator movement

shall be determined by exercising the valve while observing an appropriate

indicator.

Analysis. The inspectors determined that the performance deficiency was more than

minor because it was associated with the procedure quality attribute of the Mitigating

System cornerstone and adversely affected the cornerstone objective to ensure the

reliability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the test criterion used in procedure 2-PT-Q013A did not

ensure that valve 755A reliably performed its safety function when tested as

demonstrated by testing performed in January 2005. The inspectors determined that

the performance deficiency was of very low safety significance (Green) using IMC 0609,

Attachment 4, Phase 1 - Initial Screening and Characterization of Findings.

Specifically, the inspectors determined that this finding was of very low safety

significance because the finding did not result in a loss of safety function and did not

screen as potentially risk-significant due to external events initiating events.

The inspectors determined the finding had a cross-cutting aspect related to effective

corrective actions in the corrective action program component of the problem

identification and resolution area. Specifically, Entergy did not implement effective

corrective actions to resolve the testing inadequacy since 2005 during subsequent

quarterly testing. Additionally, the issue was considered to be indicative of current

performance because personnel when initially responding to inspector questions

concluded the acceptance criteria were adequate. (P.1(d) per IMC 0305)

Enforcement. 10 CFR 50.55a, Codes and standards, states that pumps and valves

which are classified as ASME code Class 1, Class 2, and Class 3 must meet the

inservice test requirements set forth in the ASME OM Code (2001 edition for Indian

Point Unit 2). Furthermore, inservice tests to verify operational readiness of pumps and

valves, whose function is required for safety must comply with the requirements of the

ASME OM Code. The ASME OM Code 2001 Subsection ISTC-1400 (c) states it is the

Owners responsibility to ensure that the application, method, and capability of each

nonintrusive technique is qualified. In addition, the ASME OM Code 2001 Subsection

ISTC-3530 states obturator movement shall be determined by exercising the valve

24

Enclosure

while observing an appropriate indicator. Contrary to the above, from February 2005

until February 2009, Entergy procedure 2-PT-Q031A, did not include appropriate

acceptance criteria for demonstrating operability of valve 755A. Specifically, the test did

not utilize a qualified technique for testing the check-valve and did not verify check valve

movement by observing an appropriate indicator. Because ACCP performance tests

since 2004 demonstrated satisfactory performance of the ACCPs at design flows, no

actual impact to the operability of the ACCPs was evident. Because this violation was

of very low safety significance and it was entered into Entergys corrective action

program (IP2-2009-1312), this violation is being treated as an NCV, consistent with the

NRC Enforcement Policy. NCV 2009002-06, Inadequate Test Acceptance Criteria

for Auxiliary Component Cooling Check Valves.

Cornerstone: Emergency Preparedness (EP)

1EP6 Drill Evaluation (71114.06 - 1 sample)

a.

Inspection Scope

The inspectors evaluated an emergency classification conducted on February 23, 2009,

during a licensed-operator requalification simulator training evaluation. The inspectors

observed an operating crew in the simulator respond to various, simulated initiating

events that ultimately resulted in the simulated implementation of the emergency plan.

In particular, the inspectors verified the adequacy and accuracy of the simulated

emergency classification of a Site Area Emergency. While other simulated

classifications were made, the inspectors verified that the initial classification was

appropriately credited as an opportunity toward NRC performance indicator data. The

inspectors observed the management evaluator and training critique following

termination of the scenarios, and verified that significant performance deficiencies were

appropriately identified and addressed within the critique and the corrective action

program. Also, the inspectors reviewed the summary performance report for the

evaluation and verified that appropriate attributes of drill performance including

deficiencies were captured. This evaluation constituted one inspection sample.

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

2OS1 Access Control to Radiologically Significant Areas (71121.01 - 16 samples)

a.

Inspection Scope

From March 23 through March 27, 2009, the inspectors conducted the following

activities to verify that Entergy was properly implementing physical, engineering, and

administrative controls for access to high radiation areas, and other radiologically

controlled areas, and that workers were adhering to these controls when working in

these areas. Implementation of the access control program was reviewed against the

25

Enclosure

criteria contained in 10 CFR 20, site technical specifications, and Entergys procedures

required by the Technical Specifications as criteria for determining compliance.

This inspection activity represents completion of sixteen (16) samples relative to this

inspection area. The inspector performed independent radiation dose rate

measurements and reviewed the following items:

Plant Walk Downs and Radiological Work Permit Reviews

(1)

Exposure significant work areas were identified by inspectors for review within

radiation areas, high radiation areas, and airborne areas in the plant. Associated

licensee controls and surveys were review for adequacy. Work reviewed

included: Refuel Floor Split Pin and Reactor Head Inspections, Refuel Floor

Lower Internals Removal and Installation, Refuel Floor and Fuel Support Building

Fuel Transport Equipment Repairs requiring an underwater diver, Reactor

Coolant Pump work including RCP #31 Impeller replacement, Containment valve

work including Pressurizer Safety Valves, Various Containment and Auxiliary

Building activities.

(2)

With a survey instrument and assistance from a health physics technician,

inspectors walked down the above mentioned areas to determine: whether the

radiation work permits (RWPs), procedures and engineering controls were in

place and whether surveys and postings were adequate.

(3)

The inspectors reviewed RWPs that provide access to exposure significant areas

of the plant including high radiation areas. Specified electronic personal

dosimeter alarm set points were reviewed with respect to current radiological

condition applicability and workers were queried to verify their understanding of

plant procedures governing alarm response and knowledge of radiological

conditions in their work area.

(4)

There were no radiation work permits for airborne radioactivity areas with the

potential for individual worker internal exposures of >50 mrem CEDE.

(5)

There were no internal dose assessments that resulted in actual internal

exposures greater than 50 mrem CEDE. Internal assessments were reviewed to

determine adequacy and assurance that they were not in fact equal to or greater

than 50 mrem CEDE.

Problem Identification and Resolution

(6)

Access controls related condition reports were reviewed since the last inspection

in this area. Staff members were interviewed and documents reviewed to

determine that follow-up activities are being conducted in an effective and timely

manner, commensurate with their safety and risk.

(7)

For repetitive deficiencies or significant individual deficiencies in problem

identification and resolution, the inspectors determined if the licensees

assessment activities were also identifying and addressing these deficiencies.

(8)

A review of events revealed no performance indicator occurrences that involved

dose rates greater than 25 Rem/hour at 30 cm, dose rates greater than

26

Enclosure

500 Rem/hour at 1 meter, or unintended exposures greater than 100 mrem

TEDE (or greater than 5 Rem SDE or greater than 1.5 Rem LDE)

Job-in-Progress Reviews

(9)

The inspectors observed aspects of various on-going activities to confirm that

radiological controls, such as required surveys, area postings, job coverage, and

job site preparations were conducted. The inspectors verified that personnel

dosimetry was properly worn and that workers were knowledgeable of work area

conditions. The inspectors attended pre-planning meetings for work described

earlier in the report.

(10)

Underwater diving activities associated with repairs to the fuel transport system

were reviewed for adequacy. Dosimetry requirements, bioassay requirements,

and controls were reviewed.

High Risk Significant, High Dose Rate High Radiation Areas (HRA) and Very HRA

Controls

(11)

Keys to locked and very HRA were reviewed for their controls and proper

inventory. Accessible locked HRA were verified to be properly secured and

posted during plant tours.

(12)

The inspectors discussed with Radiation Protection supervision the adequacy of

high dose rate HRA controls and procedures and verified that no programmatic

or procedural changes have occurred that reduce the effectiveness and level of

worker protection.

Radiation Worker Performance

(13)

During observation of the work activities listed above, radiation worker

performance was evaluated with respect to the specific radiation protection work

requirements and their knowledge of the radiological conditions in their work

areas.

(14)

The inspectors reviewed condition reports, related to radiation worker

performance to determine if an observable pattern traceable to a similar cause

was evident.

Radiation Protection Technician Proficiency

(15)

During observation of the work activities listed above, radiation protection

technician work performance was evaluated with respect to their knowledge of

the radiological conditions, the specific radiation protection work requirements

and radiation protection procedures.

(16)

The inspectors reviewed condition reports, related to radiation worker

performance to determine if an observable pattern traceable to a similar cause

was evident.

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Enclosure

b.

Findings

Introduction. The inspectors identified a NCV of very low safety significance (Green)

related to Technical Specification 5.4.1.a, Procedures, because Entergy personnel did

not generate condition reports or investigation paperwork for multiple high dose-rate

alarms as required by station procedures. Specifically, personnel did not generate the

required condition reports and adequately document the investigations for six instances

of unplanned or un-briefed electronic dosimeter alarms received by individuals in the

Unit 2 radiologically controlled area (RCA) that occurred between January 2009 and

March 2009.

Description. During the period January 2009 through March 2009, six instances of

electronic dosimeter dose rate alarms were recorded by the access control system for

Unit 2 personnel in the RCA (Unit 3 had 15 instances). During this period, Entergy

personnel inconsistently utilized an informal process of reviewing the alarms without a

full investigation or approval process. Moreover, in one of the six instances at Unit 2,

the inspectors identified that no investigation or follow-up had occurred. In some cases,

the occurrences were over two months old, which the inspectors noted would have

made resultant investigations more challenging to perform. In other cases, the alarms

were not identified until the worker attempted to re-enter the RCA and the access control

system required manual override to un-lock the occurrence to allow entry into the RCA.

The inspectors noted that the controlling Entergy procedure for this activity, EN-RP-203,

Dose Assessment, specifies that for a dose-rate alarm that is unanticipated or un-

briefed, several actions are required, one of which is to initiate a condition report,

another is to document the investigation using an attachment in the procedure. Contrary

to EN-RP-203, for these 21 instances, no condition reports or attachments were

generated with a detailed investigation prior to the workers re-entering the radiologically

controlled area. The highest exposure received by these workers during their entry, as

indicated by their electronic dosimeter and logged by the access control system, was 33

mRem, while most dosimeters indicated less than 1 mRem for the entry.

Analysis. The inspectors determined that the failure to generate a condition report, as

well as the failure to adequately investigate six unplanned or un-briefed electronic

dosimeter alarms prior to re-entry into the Unit 2 RCA, as required by station procedure

was a performance deficiency. This performance deficiency was within Entergy

personnels ability to foresee and correct, and should have been prevented. This issue

was not subject to traditional enforcement, in that it did not have actual safety

consequence, it was not an issue that had the potential to impact NRCs ability to

perform its regulatory function, and there were no willful aspects.

The finding is more than minor because it is associated with the Occupational Radiation

Safety cornerstone attribute of programs and process, and adversely affected its

objective to ensure adequate protection of worker health and safety from exposure to

radiation. Moreover, the inspectors identified a programmatic deficiency to maintain and

implement programs to keep exposures as low as reasonably achievable, because

multiple examples were identified regarding the failure to satisfy station radiation

protection procedures. Specifically, in six cases, Entergy did not fully evaluate dose rate

alarms received by workers in radiologically controlled areas of the plant. Using the

Occupational Radiation Safety Significance Determination Process, the inspectors

determined that the finding was of very low safety significance (Green) because it did not

involve: (1) as low as is reasonably achievable planning and controls, (2) an

28

Enclosure

overexposure, (3) a substantial potential for overexposure, or (4) an impaired ability to

assess dose.

The inspectors determined that the finding had a cross-cutting aspect related to

procedural adherence in the Work Practices component of the Human Performance

area. Specifically, Entergy employees did not follow procedures to generate condition

reports and document investigations when high-dose rate alarms were received by

workers. (H.4 (b) per IMC 0305)

Enforcement. Technical Specification 5.4.1.a, Procedures, requires that Entergy

establish, implement, and maintain procedures specified in Regulatory Guide (RG) 1.33,

Revision 2, Appendix A., Section 7.e, radiation protection procedures for personnel

monitoring. Entergy procedure EN-RP-203, Revision 2, Section 5.11, requires that a

condition report be written for each unplanned or un-briefed electronic dosimeter dose-

rate alarm. Contrary to the above, the inspectors identified through a review of

electronic dosimeter log information from January 2009 through March 2009, six

instances of unanticipated or un-briefed electronic dosimeter dose-rate alarms when the

procedure was not implemented and condition reports were not generated. Because

this finding was of very low safety significance and it was entered into the corrective

action program as CR-IP3-2009-001253 and CR-IP3-2009-001318, this violation is

being treated as an NCV, consistent with the NRC Enforcement Policy. NCV 05000247/2009002-07, Failure to Follow Radiation Protection Procedures.

2OS2 ALARA Planning and Controls (71121.02 - 12 samples)

a.

Inspection Scope

From March 23 through March 27, 2009, the inspectors conducted the following

activities to verify that Entergy was properly maintaining individual and collective

radiation exposures as low as is reasonably achievable (ALARA). Implementation of the

ALARA program was reviewed by inspectors against the criteria contained in 10 CFR

20, applicable industry standards, and Entergys procedures.

This inspection activity represents completion of twelve (12) samples relative to this

inspection area.

Inspection Planning

(1)

The inspectors reviewed pertinent information regarding cumulative exposure

history, current exposure trends, and on-going activities to assess current

performance and outage exposure challenges. The inspectors determined the

sites 3-year rolling collective average exposure.

(2)

The inspectors reviewed unit 3 outage work related activities occurring during the

inspection period, the associated ALARA plans, RWPs, ALARA Committee

Reviews, exposure estimates, actual exposures and post job reviews. Work

reviewed included: Refuel Floor Split Pin and Reactor Head Inspections, Refuel

Floor Lower Internals Removal and Installation, Refuel Floor and Fuel Support

Building Fuel Transport Equipment Repairs requiring an underwater diver,

Reactor Coolant Pump work including RCP #31 Impeller replacement,

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Enclosure

Containment valve work including Pressurizer Safety Valves, Various

Containment and Auxiliary Building activities.

(3)

The inspectors reviewed implementing procedures associated with maintaining

occupational exposures ALARA. This included a review of the processes used to

estimate and track work activity exposures.

Radiological Work Planning

(4)

With respect to the work activities listed above, the inspectors reviewed dose

summary reports, related post-job ALARA reviews, related RWPS, exposure

estimates and actual exposures, and ALARA Committee meeting paperwork.

Through this review, the inspector determined that dose was appropriately

managed and evaluated by Station Management.

(5)

ALARA work activity evaluations, exposure estimates, and exposure mitigating

requirements were reviewed for work packages previously mentioned. The

inspectors determined that Entergy established procedures, engineering and

work controls, based on sound radiation protection principles.

(6)

The inspectors compared the results achieved with the intended dose that was

established in the planning of the work. The inspectors determined the reasons

for any inconsistencies between the intended and actual work activity doses and

station management awareness and involvement.

(7)

The inspectors evaluated for adequacy, the interfaces between operations,

radiation protection, maintenance, maintenance planning and others for interface

problems or missing program elements.

Verification of Dose Estimates and Exposure Tracking Systems

(8)

Methods for adjusting exposure estimates, or re-planning work, when

unexpected changes in scope or emergent work is encountered, was reviewed

by the inspectors for adequacy.

Job Site Inspections and ALARA Controls

(9)

The inspectors reviewed work activities that present the highest radiological risk

to workers. The inspectors evaluated Entergys use of engineering controls to

achieve dose reductions and to verify that procedures and controls are consistent

with ALARA reviews. Associated ALARA Plans and RWPs were reviewed to

determine if appropriate exposure and contamination controls were being

employed.

Radiation Worker Performance

(10)

Through observations and interviews, workers and technicians were found to be

knowledgeable of the work area radiological conditions and low dose waiting

areas.

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Enclosure

Declared Pregnant Workers

(11)

The inspectors reviewed information associated with declared pregnant workers

during the assessment period and whether appropriate monitoring and controls

were being utilized to ensure compliance with 10CFR Part 20.

Problem Identification and Resolution

(12)

The inspectors reviewed elements of the Entergys corrective action program

related to implementing radiological controls to determine if problems are being

entered into the program for timely resolution.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES [OA]

4OA1 Performance Indicator Verification (71151 - 3 samples)

a.

Inspection Scope

The inspectors reviewed performance indicator data for the cornerstones listed below

and used Nuclear Energy Institute 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 5, to verify individual performance indicator accuracy and

completeness. The documents reviewed during this inspection are listed in the

Attachment.

Initiating Events Cornerstone

Unplanned Scrams per 7000 Critical Hours (January 2008 to December 2008)

Unplanned Transients per 7000 Critical Hours (January 2008 to December 2008)

The inspectors reviewed data and plant records from January 2008 to December 2008.

The records included PI data summary reports, licensee event reports, operator

narrative logs, Entergys corrective action program, and Maintenance Rule records. The

inspectors verified the accuracy of the number of critical hours reported, and interviewed

the system engineers and operators responsible for data collection and evaluation.

Barrier Integrity Cornerstone

RCS Activity (January 2008 to December 2008)

The inspectors reviewed data and plant records from January 2008 to December 2008.

The records included performance indicator data summary reports, licensee event

reports, operator narrative logs, Entergys corrective action program, and Maintenance

Rule records. The inspectors verified the accuracy of the number of critical hours

reported, and interviewed the system engineers and operators responsible for data

collection and evaluation.

31

Enclosure

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Problem Identification & Resolution Program Review

a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and to identify repetitive equipment failures or specific human performance issues for

follow-up, the inspectors performed a daily screening of all items entered into Entergys

corrective action program. The review was accomplished by accessing Entergys

computerized database for condition reports, and attending condition report screening

meetings.

In accordance with the baseline inspection modules, the inspectors selected corrective

action program items across the Initiating Events, Mitigating Systems, and Barrier

Integrity cornerstones for further follow-up and review. The inspectors assessed

Entergys threshold for problem identification, adequacy of the causal analysis, extent of

condition reviews, and operability determinations, and timeliness of the associated

corrective actions. The condition reports reviewed during this inspection are listed in the

Attachment.

b.

Findings

No findings of significance were identified

4OA3 Event Followup

.1

Condensate Return Line Leak on February 15, 2009

a.

Inspection Scope

On February 15, 2009, an operator observed indications of wetness in a pipe sleeve in

the floor of the auxiliary feed pump building. The operator notified the control room.

Chemistry samples of the water were drawn and analyzed. On February 16, Entergy

determined the chemistry results indicated the water was from the condensate storage

tank (CST) return line. The inspectors reviewed the technical specifications (TS) to

determine whether operators entered the applicable TS action statements for the CST

and completed required actions to administratively determine the back-up on-site city

water tank was available, if needed, to provide water to the auxiliary feedwater pumps.

The inspectors reviewed Entergys operability evaluation of the CST to determine

whether it was technically supported. In addition, the inspectors reviewed the impact of

the leak on the auxiliary feed water system which utilizes the CST as a primary source of

water and circulates water back to the CST through the CST return piping. The

inspectors also reviewed chemistry and radiological samples taken of the water to assess

the environmental impact of the leak and determine if the release was below NRC

regulatory limits for liquid effluents.

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Enclosure

b.

Findings and Observations

No findings of significance were identified.

Entergy excavated a portion of the CST piping in the area of the identified leakage and

determined that the CST return pipe was leaking due to a hole the pipe where a small

area of a protective coating was missing. Entergy also identified two additional areas of

piping with metal loss that did not exceed ASME Code minimum required wall thickness.

However, the areas were repaired while the opportunity existed. Entergy removed the

portion of pipe with the localized defects and sent the specimen to a laboratory for

analysis to identify the causes. The inspectors determined that the actions Entergy

implemented to evaluate and repair the leaking CST pipe to restore operability to the

CST were adequate and in accordance with their operating license. Additionally, the

inspectors determined that the evaluations and actions Entergy performed to evaluate

and maintain operability of the auxiliary feed pumps were adequate. Entergy analyzed

the water leaking up through the sleeve and determined it was CST water based on

hydrazine and tritium levels. The amount of tritium detected in the water was consistent

with that found in the CST, for example, analyses of samples of water from the leak

returned 2000 - 2300 picocuries per liter (pCi/l). The release was determined to be

below the NRC regulatory limits for liquid effluents. For added perspective, while not

drinking water, the Environmental Protection Agency environmental limit for drinking

water requires tritium levels less than 20,000 pCi/l.

Entergy initiated a root cause analysis to determine causes of the leak that is scheduled

to be completed in May 2009. At the end of the inspection period, the inspectors were

monitoring the performance of Entergy in implementing its corrective action program to

address the issue and develop a root cause evaluation and further corrective actions.

4OA5 Other Activities

.1

Continued Groundwater Sampling Effort to Monitor Tritium (Deviation Memorandum

Inspection)

a.

Inspection Scope

During the week of March 23-27, 2009, the inspectors met with Entergy representatives

to review the results of recent groundwater samples, as well as those taken and

analyzed in 2008. The review was conducted against criteria contained in 10CFR20,

10CFR50, and applicable industry standards.

The review of the data included a comparison of Entergys data with split samples taken

by the NRC of monitoring wells MW-66 and MW-67, as well as the LaFarge sample

point. In all, 47 samples were analyzed and compared from January 2008 through

January 2009. Isotopic analyses were performed and compared at each of the sample

points for: Tritium, Strontium 90, Nickel 63, and gamma emitters such as Cobalt-60 and

Cesium-137. Results of the NRC samples can be found in ADAMS accession numbers:

ML081420676, ML082690244, ML082690202, ML082690237, ML082730830,

ML082730810, ML090400523, ML090400516, ML090400502, ML090923932,

ML090920949.

33

Enclosure

Entergy=s evaluation of recent groundwater results are documented in condition reports:

CR-IP2-2009-00883, CR-IP2-2009-01110, CR-IP2-2009-01111, CR-IP2-2009-01113,

and CR-IP2-2009-01114.

b.

Findings

No findings of significance were identified.

The inspectors concluded that overall, there was agreement between Entergy

personnels results and those independently analyzed by the NRC, and that actions

taken by Entergy have been appropriate. The inspectors also noted that conservative

estimates indicate that the samples represent a very small fraction of the permissible

public dose limits and are negligible with respect to natural background radiation levels.

.2

Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that these activities were consistent with Entergy

security procedures and applicable regulatory requirements. Although these

observations did not constitute additional inspection samples, the inspections were

considered an integral part of the normal, resident inspector plant status reviews during

implementation of the baseline inspection program.

b.

Findings

No findings of significance were identified.

4OA6 Meetings

Exit Meeting Summary

On April 15, 2009, the inspectors presented the inspection results to Joe Pollock and

other Entergy staff members, who acknowledged the inspection results presented.

Entergy did not identify any material as proprietary.

ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Entergy Personnel

J. Pollock,

Site Vice President

A. Vitale,

General Manager, Plant Operations

P. Conroy,

Director of Nuclear Safety Assurance

A. Williams, Site Operations Manager

B. Sullivan,

Emergency Planning Manager

S. Verrochi, System Engineering Manager

R. Walpole,

Licensing Manager

D. Loope,

Manager, Radiation Protection

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed 05000247/2009002-01 FIN

Failure to Identify Open Louvers in 11 Fire

Pump House (Section 1R01)05000247/2009002-02 NCV

Failure to Identify Damaged Components in

EDG Ventilation Motor Control Center #2

(Section 1R05)05000247/2009002-03 NCV

Failure to identify and Promptly Correct

Degraded 480 Volt Switchgear Room Fire

Door (Section 1R05)05000247/2009002-04 NCV

Inadequate Maintenance Procedure for

EDG Ventilation Motor Control Center #2

(Section 1R12)05000247/2009002-05 NCV

Failure to Include RWST Level

Maintenance In Online Risk Assessment

(Section 1R13)05000247/2009002-06 NCV

Inadequate Test Acceptance Criteria for

Auxiliary Component Cooling Check Valves

(Section 1R22)05000247/2009002-07

NCV

Failure to Follow Radiation Protection

Procedures (Section 2OS1)

A-2

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

OAP-048, Rev. 4, Seasonal Weather Preparation

OAP-008, Rev. 5, Severe Weather Preparations

2-AOP-SSD-1, Rev. 13, Control Room Inaccessibility Safe Shutdown Control

OAP-017, Rev. 5, Plant Surveillance and Operator Rounds

EN-OP-115, Rev. 5, Conduct of Operations

Condition Reports

IP2-2009-00197

IP2-2009-00207

IP2-2009-00208

IP2-2009-00211

IP2-2009-00212

IP2-2009-00214

IP2-2009-00215

IP2-2009-00226

Orders

00152922

00153082

00153083

00179583

Section 1R04: Equipment Alignment

Procedures

2-PT-M103, Rev. 2, Auxiliary Feedwater System Monthly Alignment Verification

2-COL-4.1.1, Rev. 22, Component Cooling System

Section 1R05: Fire Protection

Procedures

SAO-703, Rev. 25, Fire Protection Impairment Criteria and Surveillance

EN-DC-161, Rev. 2, Control of Combustibles

OAP-037, Rev. 2, Operations Electrical Equipment Operating Guidelines

IP-SMM-IS-103, Rev. 0, IPEC Site Management Manual Electrical Safety

2-PT-SA020, Rev. 0, Swing Fire Doors

Condition Reports

IP2-2009-00904

IP2-2009-00526

IP2-2009-00680

IP2-2009-00709

IP2-2009-00834

IP2-2009-00342

IP2-2009-00483

IP2-2004-05336

IP2-2007-03561

IP2-2007-04645

IP2-2008-05447

Orders

51645822

51676572

Miscellaneous

Indian Point Nuclear Generating Station, Unit 2, Fire Protection Program Plan, Rev. 9

Indian Point Pre-Fire Plans Unit 2 - Nuclear

IP2-RPT-03-00015, IP2 Fire Hazards Analysis, Rev. 3

1R07: Heat Sink Performance

Procedures

SEP-SW-001, NRC Generic Letter 89-13 Service Water Program

PT-2Y10B, 22 CCW HX Test

2-HTX-004-CCW, Component Cooling Water Heat Exchanger Maintenance

A-3

Attachment

Work Orders

51675733

Condition Reports

IP2-2005-0673

IP2-2005-0768

IP2-2005-1268

IP2-2006-7126

IP2-2006-3974

Miscellaneous

EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines

Preliminary Report of Eddy Current Testing dated 2/10/09

21 CCW Hx Inspection Reports dated 2/23/2005 and 1/8/2007

22 CCW Hx Inspection Reports dated 2/23/2005 and 12/12/2006

Section 1R11: Licensed Operator Requalification Program

Procedures

OAP-033, Conduct of Operations Simulator Training, Evaluations, and Debriefs, Rev. 4

OAP-032, Operations Training Program, Rev. 9

2-E-0, Rev. 0, Reactor Trip or Safety Injection

2-ECA-0.0, Rev. 3, Loss of All AC Power

2-AOP-480V-1, Rev. 5, Loss of Normal Power to any 480V Bus

Miscellaneous

LRQ-SES-21, Rev. 0, IPEC Evalauted Scenario for Loss of All AC Power

Section 1R12: Maintenance Effectiveness

Procedures

2-MCC-003-ELC, Rev 0, Klockner-Moeller, Series 200, 480 Volt Motor Control Center

Preventive Maintenance

2-PC-Q2, Rev. 19, Refueling Water Storage Tank Level

0-MS-412, Rev. 0, Inspection and Cleaning of Bus Bars, Contacts, Ground Connections, Wiring

and Insulators

IP-SMM-IS-103, Rev. 0, IPEC Site Management Manual Electrical Safety

0-GNR-404-ELC, Rev. 1, Emergency Diesel Generator 2-Year Inspection

2-GNR-015-ELC, Rev. 2, Emergency Diesel Generator Preventive Maintenance 2-Year

2-PT-M021B, Rev. 17, Emergency Diesel Generator 22 Load Test

Condition Reports

IP2-2009-00527

IP2-2009-00532

IP2-2009-01041

IP2-2003-00948

IP2-2009-00342

IP2-2009-00483

IP2-2004-03106

IP2-2007-01893

IP2-2008-05382

IP2-2009-00486

IP2-2009-00041

IP2-2009-00178

IP2-2006-04101

IP2-2009-00093

IP2-2007-03476

IP2-2007-04921

IP2-2008-00454

IP2-2008-00907

IP2-2008-03976

Orders

51557262

51676147

06-16146

51696697

51322921

51268313

00181009

00167536

04-26645

57696714

51649505

51654261

00118733

07-03476

07-04921

08-00454

08-00907

09-00532

Drawing

309030-02, Loop diagram RWST level indication

3WS-463-610-14-20101-3, Schematic for EDG HVAC Heater

A-4

Attachment

IP2-S-000231-04, Schematic for EDG Building Ventilation Distribution

B248513-12, 480V MCC 26C and CCR Ventilation Distribution

B228434-02, Class A Boundary for Electrical Systems

Miscellaneous

Maintenance Rule Basis Document Residual Heat Removal System, dated 5/23/05

Maintenance Rule Basis Document HVAC Emergency Diesel Building, dated 5/23/05

IP-SMM-AD-102, Att 10.2, dated 4/6/08, for revision to procedure 2-MCC-003-ELC

Vendor Manual, Klockner-Moeller Series 200 Motor Control Center

Vendor Manual, Qmark MUH Series Modular Unit Heaters

Vendor Manual, ALCO Fuel Injection Nozzle and Holder

Maintenance Rule Expert Panel Meeting Minutes dated 2/14/05

Tagout 2-480V-Panel-MCC26C dated 4/3/08

DRN-08-01336 dated 4/6/08 for procedure 2-MCC-003-ELC

PMCR ER-06-33534, to establish maintenance activity for EDG HVAC MCC

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

IP-SMM-WM-101, On-Line Risk Assessment

2-PC-Q109, Recalibration of Nis and OT/OP delta T parameters

PT-Q17A, Verify ASSS supply to 21 AFP

2-PT-Q027A, 21 Auxiliary Feed Pump

2-PC-Q2, Rev. 19, Refueling Water Storage Tank Level

2-ES-1.3, Rev. 2, Transfer to Cold Leg Recirculation

Condition Reports

IP2-2009-00018

IP2-2009-00027

IP2-2009-00139

IP2-2009-00143

IP2-2009-00148

IP2-2009-00389

Work Orders

00165604

51654961

51692571

51692351

51696697

Miscellaneous

Equipment Out-Of-Service (EOOS) risk assessment reports

Section 1R15: Operability Evaluations

Procedures

2-PT-Q031A, 21 Auxiliary Component Cooling Pump

2-PT-Q031B, 22 Auxiliary Component Cooling Pump

EN-MA-133, Control of Scaffolding

2-AOP-IB-1, Loss of Power to an Instrument Bus

2-PT-M021B, Rev. 17, Emergency Diesel Generator 22 Load Test

2-SOP-AFW-002, Rev. 1, Auxiliary Feedwater System Operation Support Procedure

Drawings

A249955-21, 480V AC MCC 29 & 29A

Calculation

IP3-CALC-FW-01482, Rev. 0, Feedwater Stratification and Auxiliary Feedwater

A-5

Attachment

Condition Reports

IP2-2009-0500

IP2-2009-0505

IP2-2008-3749

IP2-2009-0547

IP2-2009-0567

IP2-2009-0509

IP2-2005-0252

IP2-2009-0552

IP2-2009-0655

IP2-2008-2705

IP2-2009-0041

IP2-2009-0093

Work Orders

NP-99-07694

Miscellaneous

WCAP-12312, Rev. 2, Safety Evaluation for an Ultimate Heat Sink Temperature Increase to 95F

at Indian Point Unit 2

Heat exchanger data sheet for containment recirculation pump number 22 motor cooler

WCAP-7829, Fan Cooler Motor Unit Test

Environmental Qualification Report for Containment Recirculation Pump Motors

IP2-CCW-DBD, Component Cooling Water design bases document

IP2-DBD-207, Design Basis Document for 118V AC Electrical System

AMSE OM-2001 Edition

Unit 2 active scaffold list

VM 1073-1.2, Vendor manual for auxiliary component cooling pumps

VM 1100, vendor manual for 118V AC solid state static inverters

Work order NP-89-43777, replacement of 22 ACCP impeller

IP2-AFW-DBD, Rev. 1, AFW Design Basis Document

Section 1R18: Plant Modifications

Procedures

2-SOP-18-1, Main and Reheat Steam System

TP-SQ-11.016, Post Work Test Program (historical)

Condition Reports

IP2-2009-0983

IP2-2009-0137

IP2-2008-5636

IP2-2009-0077

IP2-2009-0069

IP2-2009-0062

IP2-2008-5621

IP2-2009-0781

Work Orders

IP2-03-11725

IP2-02-32013

51305160

Drawings

B235623-6, Atmospheric Steam Dump Panel

9321-F-70313, Auxiliary Boiler Feed Pump Room Instrument Piping

Miscellaneous

IP2 Maintenance Rule Basis for Main Steam System

IP2-MS-DBD, Design Basis Document for the Main Steam System

IPT-RPT-05-00071, Appendix R Safe Shutdown Analysis

SEE-03-5, Indian Point Unit 2 RHR Cooldown Analysis for the 5% Power Uprate

IP2 Inservice Testing Program Basis Data Sheets for PCV-1136 & 1137 (23/24 SG ADVs)

ER 06-2-012, Install Secondary Backup Nitrogen Cylinders at both S/G ADV Local Control

Panels in the ABFP Building

A-6

Attachment

Section 1R19: Post-Maintenance Testing

Procedures

OAP-24, Operations Testing, Rev. 3

2-PT-M021C, Rev. 16, Emergency Diesel Generator 23 Load Test

0-GNR-403-ELC, Emergency Diesel Generator Quarterly Inspection

2-PT-Q033B, 21 Charging Pump

2-SOP-4.1.2, Rev. 34, Component Cooling System Operation

Orders

51797559

51797558

52027651

00183296

00157710

51675732

Section 1R22: Surveillance Testing

Procedures

2-PT-2M4, Safety Injection System Train A Actuation Logic and Master Relay Test

2-PT-Q013, Inservice Valve Tests

2-PT-Q013-DS027, Valve 888A IST Data Sheet

0-SOP-LEAKRATE-001, Rev. 1, RCS Leakrate Surveillance, Evaluation and Leak Identification

2-PT-Q030C, Rev. 18, 23 Component Cooling Water Pump

Drawings

11497, Valve 888A

Condition Reports

IP2-2007-1754

IP2-2008-1443

IP2-2008-2002

IP2-2007-3329

Orders

51694305

Miscellaneous

IP2-ESF DBD, Design Basis Document for Engineered Safeguards Features System

IP2 Inservice Testing Program Data Sheet - Valve 888A

PGI-00066-01, 888 A & B Diff Pr Calc

Section 1EP6: Drill Evaluation

Procedures

IP-EP-120, Rev. 3, Emergency Classification

Miscellaneous

IP-EP-115, Rev. 24, form EP-1 radiological emergency data forms dated 2/23/09

Section 2OS1: Access Control to Radiologically Significant Areas and

Section 2OS2: ALARA Planning and Controls

Procedures

EN-RP-100, Rev. 03, Radworker Expectations

EN-RP-101, Rev. 04, Access Control for Radiologically Controlled Areas

EN-RP-102, Rev. 02, Radiological Control

EN-RP-105, Rev. 04, Radiation Work Permits

EN-RP-108, Rev. 07, Radiation Protection Posting

EN-RP-110, Rev. 05, ALARA Program

A-7

Attachment

EN-RP-121, Rev. 04, Radioactive Material Control

EN-RP-131, Rev. 06, Air Sampling

EN-RP-141, Rev. 04, Job Coverage

EN-RP-151, Rev. 02, Radiological Diving

EN-RP-202, Rev. 06, Personnel Monitoring

EN-RP-203, Rev. 02, Dose Assessment

EN-RP-204, Rev. 02, Special Monitoring Requirements

EN-RP-205, Rev. 02, Prenatal Monitoring

EN-RP-208, Rev. 02, Whole Body Counting and In-Vitro Bioassay

Condition Reports

CR-IP3-2009-00752, CR-IP3-2009-00785, CR-IP3-2009-00857, CR-IP3-2009-00885

CR-IP3-2009-00886, CR-IP3-2009-00937, CR-IP3-2009-00998, CR-IP3-2009-01006

CR-IP3-2009-01107, CR-IP3-2009-01154, CR-IP3-2009-01169, CR-IP3-2009-01171

CR-IP3-2009-01183, CR-IP3-2009-01253, CR-IP3-2009-01293, CR-IP3-2009-01295

CR-IP3-2009-01296, CR-IP3-2009-01318, CR-IP2-2009-00883, CR-IP2-2009-01110,

CR-IP2-2009-01111, CR-IP2-2009-01113, CR-IP2-2009-01114

Miscellaneous

Radiation Protection Attention Logs (Electronic Dosimeter Alarms)

TEDE ALARA Evaluations

ALARA Committee Reviews

RP-STD-XX, Rev. X, Unreported Dosimeter Alarms and Anomolies (Draft)

IPEC Snapshot Self-Assessment Report (IP3-LO-2007-0010) July 2007 - June 2008.

RWPs: 2009-002, 2009-003, 2009-2021, 2009-3001, , 2009-3002, 2009-3056, 2009-3501,

2009-3504, 2009-3515, 2009-3529

Section 4OA1: Performance Indicator Verification

EN-EP-201, "Performance Indicators," Rev. 6

EN-LI-114, Performance Indicator Process, Rev. 3

NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 5

0-CY-2765, Rev. 3, Coolant Activity Limits

Section 4OA2: Identification and Resolution of Problems

Procedures

EN-LI-102, Rev. 13, Corrective Action Process

Condition Reports

IP2-2009-00342

IP2-2009-00483

IP2-2004-03106

IP2-2007-01893

IP2-2008-05382

IP2-2009-00486

IP2-2009-00027

IP2-2009-00139

IP2-2009-00143

IP2-2009-00148

A-8

Attachment

LIST OF ACRONYMS

ALARA

as low as is reasonably achievable

ABFW

auxiliary boiler feedwater

ABFP

auxiliary boiler feedwater pump

ACCP

auxiliary component cooling pump

ADAMS

Agency-wide Document and Management System

ASME

American Society of Mechanical Engineers

CAP

corrective action program

CCW

component cooling water

CDF

core damage frequency

CFR

Code of Federal Regulations

CST

condensate storage tank

EDO

Executive Director of Operations

EDG

emergency diesel generator

ENTERGY

Entergy Nuclear Northeast

EP

Emergency Preparedness

HRA

high radiation area

IMC

Inspection Manual Chapter

IPEC

Indian Point Energy Center

IST

in-service test

MCC

motor control center

NCV

non-cited violation

NDE

non-destructive examination

NRC

Nuclear Regulatory Commission

NRR

Nuclear Reactor Regulation

NSR

non safety-related

PARS

Publicly Available Records System

PI

performance indicator

RCA

radiologically controlled area

RCS

reactor coolant system

RWP

radiation work permit

RWST

refueling water storage tank

SDP

significance determination process

SER

safety evaluation report

SG

steam generator

SR

safety related

SSC

structures, systems, and components

TS

Technical Specification

UFSAR

Updated Final Safety Evaluation Report

URI

unresolved item

WO

work order