IR 05000387/2007005: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:February 14, 2008 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Paul G. Krohn, Chief Projects Branch 4 Division of Reactor Projects Docket Nos. 50-387; 50-388 License Nos. NPF-14, NPF-22 | |||
Paul G. Krohn, Chief Projects Branch 4 Division of Reactor Projects | |||
Docket Nos. | |||
50-387; 50-388 License Nos. NPF-14, NPF-22 | |||
===Enclosures:=== | ===Enclosures:=== | ||
Inspection Report 05000387/2007005 and 05000388/2007005 Attachment: Supplemental Information | Inspection Report 05000387/2007005 and 05000388/2007005 | ||
Attachment: Supplemental Information | |||
REGION I== | REGION I== | ||
Docket No: 50-387, 50-388 License No: NPF-14, NPF-22 Report No: 05000387/2007005 and 05000388/2007005 Licensee: PPL Susquehanna, LLC Facility: Susquehanna Steam Electric Station, Units 1 and 2 Location: Berwick, Pennsylvania Dates: October 1, 2007 through December 31, 2007 Inspectors: F. Jaxheimer, Senior Resident Inspector S. Hansell, Limerick Senior Resident Inspector P. Finney, Resident Inspector J. Kulp, Reactor Engineer T. OHara, Reactor Engineer J. Furia, Senior Health Physicist A. Ziedonis, Reactor Inspector Approved By: Paul G. Krohn, Chief Projects Branch 4 Division of Reactor Projects Enclosure | Docket No: | ||
50-387, 50-388 | |||
License No: | |||
NPF-14, NPF-22 | |||
Report No: | |||
05000387/2007005 and 05000388/2007005 | |||
Licensee: | |||
PPL Susquehanna, LLC | |||
Facility: | |||
Susquehanna Steam Electric Station, Units 1 and 2 | |||
Location: | |||
Berwick, Pennsylvania | |||
Dates: | |||
October 1, 2007 through December 31, 2007 | |||
Inspectors: | |||
F. Jaxheimer, Senior Resident Inspector | |||
S. Hansell, Limerick Senior Resident Inspector P. Finney, Resident Inspector | |||
J. Kulp, Reactor Engineer | |||
T. OHara, Reactor Engineer | |||
J. Furia, Senior Health Physicist | |||
A. Ziedonis, Reactor Inspector | |||
Approved By: | |||
Paul G. Krohn, Chief | |||
Projects Branch 4 | |||
Division of Reactor Projects | |||
Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
IR 05000387/2007005, 05000388/2007005; 10/01/2007 - 12/31/2007; Susquehanna Steam | IR 05000387/2007005, 05000388/2007005; 10/01/2007 - 12/31/2007; Susquehanna Steam | ||
Electric Station, Units 1 and 2; Maintenance Effectiveness and ALARA Planning and Controls. | Electric Station, Units 1 and 2; Maintenance Effectiveness and ALARA Planning and Controls. | ||
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===NRC-Identified and Self-Revealing Findings=== | ===NRC-Identified and Self-Revealing Findings=== | ||
===Cornerstone: Barrier Integrity=== | ===Cornerstone: Barrier Integrity=== | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
A self-revealing non-cited violation of 10CFR 50 Appendix B, Criterion III, | A self-revealing non-cited violation of 10CFR 50 Appendix B, Criterion III, | ||
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This finding was more than minor because the finding is related to the Design Control and Human Performance attributes of the barrier integrity cornerstone and negatively impacts the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding) protect the public from radio nuclide releases caused by accidents or events. The inspectors completed a Phase 1 significance determination using IMC 0609 Appendix A, Significance Determination Process Phase 1 screening worksheet, and determined the finding to be of Very Low Safety Significance (Green) because the performance issue only degraded the Fuel Cladding Barrier and its associated cornerstone. | This finding was more than minor because the finding is related to the Design Control and Human Performance attributes of the barrier integrity cornerstone and negatively impacts the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding) protect the public from radio nuclide releases caused by accidents or events. The inspectors completed a Phase 1 significance determination using IMC 0609 Appendix A, Significance Determination Process Phase 1 screening worksheet, and determined the finding to be of Very Low Safety Significance (Green) because the performance issue only degraded the Fuel Cladding Barrier and its associated cornerstone. | ||
This finding is related to a cross-cutting component in the area of Human Performance associated with work practices H.4.(c) because PPL did not ensure supervisory and management oversight of specific work activities, specifically design reviews which supported the fuel rechanneling procedures used from October 2005 through October 2007 and the collective evaluation of 25 condition reports related to rechanneling difficulties. PPL entered this issue into the corrective action program and promptly initiated compensatory measures to impose fuel thermal limit penalties to assure fuel barrier integrity during reactor operation. (IR12) | This finding is related to a cross-cutting component in the area of Human Performance associated with work practices H.4.(c) because PPL did not ensure supervisory and management oversight of specific work activities, specifically design reviews which supported the fuel rechanneling procedures used from October 2005 through October 2007 and the collective evaluation of 25 condition reports related to rechanneling difficulties. PPL entered this issue into the corrective action program and promptly initiated compensatory measures to impose fuel thermal limit penalties to assure fuel barrier integrity during reactor operation. (IR12) | ||
===Cornerstone: Occupational Radiation Safety=== | ===Cornerstone: Occupational Radiation Safety=== | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
A self-revealing finding having very low safety significance was identified due to a deficiency in the area of maintaining occupational radiation exposures as low as is reasonably achievable (ALARA). ALARA and work planning for the control room emergency outside air supply system (CREOAS) modification was less than adequate resulting in collective exposure for the work to expand from 3.37 person-rem to 11.9 person-rem. | A self-revealing finding having very low safety significance was identified due to a deficiency in the area of maintaining occupational radiation exposures as low as is reasonably achievable (ALARA). ALARA and work planning for the control room emergency outside air supply system (CREOAS) modification was less than adequate resulting in collective exposure for the work to expand from 3.37 person-rem to 11.9 person-rem. | ||
The performance deficiency that resulted in the exposure overrun was due to significantly increased hours beyond that planned to perform the work. The root cause of the overrun was determined to be: (1) a failure to include contractor work hours in the ALARA planning process; and (2) design errors which did not properly identify bolting locations for the duct work, requiring extensive on-site rework. Susquehannas three-year rolling average is 101 Person-rem, which is below the SDP criteria of 240 person-rem for Boiling Water Reactors (BWRs), | The performance deficiency that resulted in the exposure overrun was due to significantly increased hours beyond that planned to perform the work. The root cause of the overrun was determined to be: (1) a failure to include contractor work hours in the ALARA planning process; and (2) design errors which did not properly identify bolting locations for the duct work, requiring extensive on-site rework. Susquehannas three-year rolling average is 101 Person-rem, which is below the SDP criteria of 240 person-rem for Boiling Water Reactors (BWRs), therefore, overall ALARA performance has been effective and this finding is of very low safety significance. | ||
therefore, overall ALARA performance has been effective and this finding is of very low safety significance. | |||
A contributing cause of this finding was related to the Work Control aspect of the Human Performance cross-cutting area because the licensee did not appropriately coordinate work activities by incorporating actions to address the impact of the work on different job activities, and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant and human performance. (H.3b) | A contributing cause of this finding was related to the Work Control aspect of the Human Performance cross-cutting area because the licensee did not appropriately coordinate work activities by incorporating actions to address the impact of the work on different job activities, and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant and human performance. (H.3b) | ||
(Section 2OS2) | |||
===Licensee Identified Violations=== | ===Licensee Identified Violations=== | ||
Violations of very low safety significance, which were identified by PPL have been reviewed by the inspectors. Corrective actions taken or planned by PPL have been entered into PPL's corrective action program. These violations and corrective actions tracking numbers are listed in Section 4OA7 of this report. | Violations of very low safety significance, which were identified by PPL have been reviewed by the inspectors. Corrective actions taken or planned by PPL have been entered into PPL's corrective action program. These violations and corrective actions tracking numbers are listed in Section 4OA7 of this report. | ||
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===Summary of Plant Status=== | ===Summary of Plant Status=== | ||
Susquehanna Steam Electric Station (SSES) Unit 1 began the inspection period at full rated thermal power. The Unit 1 reactor was shutdown on October 12, 2007, for a maintenance and fuel assembly rechanneling outage. The unit was restarted on October 29, 2007, and reached full power operation on November 2, 2007. With the exception of brief power reductions to perform control rod pattern adjustments the unit operated at full power for the remainder of the inspection period. | Susquehanna Steam Electric Station (SSES) Unit 1 began the inspection period at full rated thermal power. The Unit 1 reactor was shutdown on October 12, 2007, for a maintenance and fuel assembly rechanneling outage. The unit was restarted on October 29, 2007, and reached full power operation on November 2, 2007. With the exception of brief power reductions to perform control rod pattern adjustments the unit operated at full power for the remainder of the inspection period. | ||
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==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity | Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity | ||
{{a|1R01}} | {{a|1R01}} | ||
==1R01 Adverse Weather Protection (71111.01 - 2 Samples) | |||
== | |||
===.1 Adverse Weather - Readiness for Seasonal Susceptibilities=== | ===.1 Adverse Weather - Readiness for Seasonal Susceptibilities=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
During the week of November 8, 2007, the inspectors reviewed system operations during extreme cold weather. Plant walkdowns for selected structures, systems, and components (SSCs) were performed to determine the adequacy of PPLs weather protection features. Inspectors reviewed operator actions to address failures of equipment due to freezing and compensatory actions during adverse cold weather conditions. The inspectors also reviewed and evaluated plant conditions resulting from cold weather and reviewed considerations in PPLs Maintenance Rule station risk assessment. Additional documents that were reviewed are listed in the attachment. | During the week of November 8, 2007, the inspectors reviewed system operations during extreme cold weather. Plant walkdowns for selected structures, systems, and components (SSCs) were performed to determine the adequacy of PPLs weather protection features. Inspectors reviewed operator actions to address failures of equipment due to freezing and compensatory actions during adverse cold weather conditions. The inspectors also reviewed and evaluated plant conditions resulting from cold weather and reviewed considerations in PPLs Maintenance Rule station risk assessment. Additional documents that were reviewed are listed in the attachment. | ||
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===.2 Adverse Weather - Impending Adverse Weather Conditions=== | ===.2 Adverse Weather - Impending Adverse Weather Conditions=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On December 15, 2007, during the onset of a snow and ice storm with high winds, the inspectors reviewed PPLs preparations/protection for selected risk significant SSCs exposed to the adverse outdoor conditions. The inspection focused on verifying the design features and implementation of PPLs procedures to protect the mitigating systems from adverse weather effects such that the SSCs remained operable. This included review of open work items on heat trace and other freeze protection measures, plant walkdowns of the selected SSCs, and reviews of the Final Safety Analysis Report (FSAR), Technical Specifications (TS), and plant documents for the selected SSCs. The following outdoor systems were reviewed: condensate storage tanks, fire system valves, emergency safeguards, 4KV transformers, station blackout, diesel and offsite power transformers T-10 and T-20. | On December 15, 2007, during the onset of a snow and ice storm with high winds, the inspectors reviewed PPLs preparations/protection for selected risk significant SSCs exposed to the adverse outdoor conditions. The inspection focused on verifying the design features and implementation of PPLs procedures to protect the mitigating systems from adverse weather effects such that the SSCs remained operable. This included review of open work items on heat trace and other freeze protection measures, plant walkdowns of the selected SSCs, and reviews of the Final Safety Analysis Report (FSAR), Technical Specifications (TS), and plant documents for the selected SSCs. The following outdoor systems were reviewed: condensate storage tanks, fire system valves, emergency safeguards, 4KV transformers, station blackout, diesel and offsite power transformers T-10 and T-20. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R04}} | No findings of significance were identified. {{a|1R04}} | ||
==1R04 Equipment Alignment (71111.04 - 4 Samples) | |||
== | |||
===.1 Partial Walkdown=== | ===.1 Partial Walkdown=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed partial walkdowns to verify system and component alignment and to identify any discrepancies that would impact system operability. The inspectors verified that selected portions of redundant or backup systems or trains were available while certain system components were out of service. The inspectors reviewed selected valve positions, electrical power availability, and the general condition of major system components. The walkdowns included the following systems: | The inspectors performed partial walkdowns to verify system and component alignment and to identify any discrepancies that would impact system operability. The inspectors verified that selected portions of redundant or backup systems or trains were available while certain system components were out of service. The inspectors reviewed selected valve positions, electrical power availability, and the general condition of major system components. The walkdowns included the following systems: | ||
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===.2 Complete Walkdown=== | ===.2 Complete Walkdown=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted a detailed review of the alignment and condition of the Unit 1 Reactor Core Isolation Cooling System (RCIC). The inspectors reviewed operator rounds, check-off lists, system operating procedures, and system piping and instrumentation diagrams. The inspectors evaluated ongoing maintenance and outstanding condition reports associated with the RCIC system to determine the effect on system health and reliability. The walkdown included the following system: | The inspectors conducted a detailed review of the alignment and condition of the Unit 1 Reactor Core Isolation Cooling System (RCIC). The inspectors reviewed operator rounds, check-off lists, system operating procedures, and system piping and instrumentation diagrams. The inspectors evaluated ongoing maintenance and outstanding condition reports associated with the RCIC system to determine the effect on system health and reliability. The walkdown included the following system: | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R05}} | No findings of significance were identified. {{a|1R05}} | ||
==1R05 Fire Protection (71111.05 - 9 Samples) | |||
== | |||
===.1 Fire Protection - Tours=== | ===.1 Fire Protection - Tours=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed PPLs fire protection program to evaluate the required fire protection design features, fire area boundaries, and combustible loading requirements for selected areas. The inspectors walked down those areas to assess PPLs control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures to assess PPL's fire protection program in those areas. The inspected areas included: | The inspectors reviewed PPLs fire protection program to evaluate the required fire protection design features, fire area boundaries, and combustible loading requirements for selected areas. The inspectors walked down those areas to assess PPLs control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures to assess PPL's fire protection program in those areas. The inspected areas included: | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R06}} | No findings of significance were identified. {{a|1R06}} | ||
==1R06 Flood Protection Measures (71111.06 - 1 Sample) | |||
== | |||
===.1 Internal Flooding=== | ===.1 Internal Flooding=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed documents, interviewed plant personnel, and walked down SSCs to evaluate the adequacy of PPLs internal flood protection measures. The inspection focused on verifying that PPLs flooding mitigation plans and equipment were consistent with the design requirements and risk analysis assumptions. The material condition of credited components such as watertight plugs, floor drains, flood detection equipment and alarms were also assessed to determine whether the components were capable of performing their intended function. The inspectors also verified that adequate procedures were in place to identify and respond to floods. The following risk significant area was reviewed: | The inspectors reviewed documents, interviewed plant personnel, and walked down SSCs to evaluate the adequacy of PPLs internal flood protection measures. The inspection focused on verifying that PPLs flooding mitigation plans and equipment were consistent with the design requirements and risk analysis assumptions. The material condition of credited components such as watertight plugs, floor drains, flood detection equipment and alarms were also assessed to determine whether the components were capable of performing their intended function. The inspectors also verified that adequate procedures were in place to identify and respond to floods. The following risk significant area was reviewed: | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R07}} | No findings of significance were identified. {{a|1R07}} | ||
==1R07 Heat Sink Performance (71111.07A - 1 Sample) | |||
==1R07 Heat Sink Performance (71111.07A - 1 Sample) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed PPLs programs for maintenance, testing, and monitoring of risk significant heat exchangers (HXs) to determine whether potential HX deficiencies could mask degraded performance, and to assess the capability of the HXs to perform their design functions. The inspectors assessed whether Susquehannas HX programs conformed to PPLs commitments to NRC Generic Letter 89-13, "Service Water (SW) | The inspectors reviewed PPLs programs for maintenance, testing, and monitoring of risk significant heat exchangers (HXs) to determine whether potential HX deficiencies could mask degraded performance, and to assess the capability of the HXs to perform their design functions. The inspectors assessed whether Susquehannas HX programs conformed to PPLs commitments to NRC Generic Letter 89-13, "Service Water (SW) | ||
System Problems Affecting Safety-Related Equipment." In addition, the inspectors evaluated whether any potential common cause heat sink performance problems could affect multiple HXs in mitigating systems or result in an initiating event. Based on risk significance and prior inspection history, the following HXs were selected: | System Problems Affecting Safety-Related Equipment." In addition, the inspectors evaluated whether any potential common cause heat sink performance problems could affect multiple HXs in mitigating systems or result in an initiating event. Based on risk significance and prior inspection history, the following HXs were selected: | ||
C | |||
C Unit 1, reactor core isolation cooling (RCIC) system lube oil cooler, IE21. | |||
The inspectors assessed the external condition of the HXs in the field; reviewed the most recent eddy current data results; inspection and cleaning work results; and reviewed the applicable system heath reports to confirm that results were acceptable and that design basis assumptions for flow rate, plugged tube percentage, and heat transfer capability had been met. | The inspectors assessed the external condition of the HXs in the field; reviewed the most recent eddy current data results; inspection and cleaning work results; and reviewed the applicable system heath reports to confirm that results were acceptable and that design basis assumptions for flow rate, plugged tube percentage, and heat transfer capability had been met. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified | No findings of significance were identified | ||
{{a|1R11}} | {{a|1R11}} | ||
==1R11 Licensed Operator Requalification Program (71111.11 - 1 Sample) | |||
==1R11 Licensed Operator Requalification Program (71111.11 - 1 Sample) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On December 21, 2007, the inspectors observed licensed operator simulator training during routine operator requalification training. The inspectors compared their observations to TSs, emergency plan implementation, and the use of system operating procedures. The inspectors also evaluated PPLs critique of the operators' performance to identify discrepancies and deficiencies in operator training. The following training was observed: | == | ||
C | On December 21, 2007, the inspectors observed licensed operator simulator training during routine operator requalification training. The inspectors compared their observations to TSs, emergency plan implementation, and the use of system operating procedures. The inspectors also evaluated PPLs critique of the operators' performance to identify discrepancies and deficiencies in operator training. The following training was observed: | ||
C An operating crew simulator scenario that included a simulated failure of the reactor to scram, trip of both control rod drive pumps, trip of the A standby liquid control pump, and the inadvertent closure of the main steam isolation valves. | |||
The scenario included the proper emergency plan Site Area Emergency event classification. | The scenario included the proper emergency plan Site Area Emergency event classification. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R12}} | No findings of significance were identified. {{a|1R12}} | ||
==1R12 Maintenance Effectiveness (71111.12 - 1 Sample) | |||
==1R12 Maintenance Effectiveness (71111.12 - 1 Sample) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors evaluated PPLs work practices and follow-up corrective actions for selected SSC issues to assess the effectiveness of PPL's maintenance activities. The inspectors reviewed the performance history of those SSCs and assessed PPLs extent of condition determinations for these issues with potential common cause or generic implications to evaluate the adequacy of PPLs corrective actions. The inspectors reviewed PPL's problem identification and resolution actions for these issues to evaluate whether PPL had appropriately monitored, evaluated, and dispositioned the issues in accordance with PPL procedures and the requirements of 10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance." In addition, the inspectors reviewed selected SSC classification, performance criteria and goals, and PPL's corrective actions that were taken or planned, to verify whether the actions were reasonable and appropriate. This review included the associated system design basis, including the Final Safety Analysis Report (FSAR), the Core Operating Limits Report, and previous documented issues with fuel rechanneling activities. In addition, the inspectors performed field walkdowns and interviewed PPL staff to verify whether the identified actions were appropriate to correct the extent of condition for identified performance issues. The following issue was reviewed: | The inspectors evaluated PPLs work practices and follow-up corrective actions for selected SSC issues to assess the effectiveness of PPL's maintenance activities. The inspectors reviewed the performance history of those SSCs and assessed PPLs extent of condition determinations for these issues with potential common cause or generic implications to evaluate the adequacy of PPLs corrective actions. The inspectors reviewed PPL's problem identification and resolution actions for these issues to evaluate whether PPL had appropriately monitored, evaluated, and dispositioned the issues in accordance with PPL procedures and the requirements of 10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance." In addition, the inspectors reviewed selected SSC classification, performance criteria and goals, and PPL's corrective actions that were taken or planned, to verify whether the actions were reasonable and appropriate. This review included the associated system design basis, including the Final Safety Analysis Report (FSAR), the Core Operating Limits Report, and previous documented issues with fuel rechanneling activities. In addition, the inspectors performed field walkdowns and interviewed PPL staff to verify whether the identified actions were appropriate to correct the extent of condition for identified performance issues. The following issue was reviewed: | ||
* Units 1 and 2, rechanneling of fuel assemblies; maintenance procedures and effectiveness of quality controls. | * Units 1 and 2, rechanneling of fuel assemblies; maintenance procedures and effectiveness of quality controls. | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
A Green self-revealing NCV of 10 CFR Appendix B, Criterion III, Design Control, was identified on December 6, 2007, when PPL maintenance personnel working on the refuel floor identified foreign material at a fuel preparation machine. The foreign material was visually identified to be the outer portions of fuel spacer grid assemblies. As part of the extent of condition investigation, additional spacer grid pieces were found at two other fuel preparation machines within the spent fuel pool (SFP). This failure of plant equipment was promptly entered into the PPL corrective action program and determined to be a Significant Condition Adverse to Quality. | A Green self-revealing NCV of 10 CFR Appendix B, Criterion III, Design Control, was identified on December 6, 2007, when PPL maintenance personnel working on the refuel floor identified foreign material at a fuel preparation machine. The foreign material was visually identified to be the outer portions of fuel spacer grid assemblies. As part of the extent of condition investigation, additional spacer grid pieces were found at two other fuel preparation machines within the spent fuel pool (SFP). This failure of plant equipment was promptly entered into the PPL corrective action program and determined to be a Significant Condition Adverse to Quality. | ||
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Based on all the information available, PPL implemented the following three compensatory measures to assure fuel barrier integrity: | Based on all the information available, PPL implemented the following three compensatory measures to assure fuel barrier integrity: | ||
* a fuel thermal limit penalty was applied which reduced the maximum fraction of limiting critical power ratio (MFLCPR) to less than or equal to 0.84 for rechanneled fuel; | * a fuel thermal limit penalty was applied which reduced the maximum fraction of limiting critical power ratio (MFLCPR) to less than or equal to 0.84 for rechanneled fuel; | ||
* a fuel thermal limit penalty was applied which reduced the ratio of the maximum linear heat generation rate (fraction design limit ratio - FDLRX) to less than or equal to 0.92 for re-channeled fuel; and | * a fuel thermal limit penalty was applied which reduced the ratio of the maximum | ||
* the function of the reactor recirculation pump high flow electrical and mechanical stops (non-safety related) were credited in the analysis. | |||
linear heat generation rate (fraction design limit ratio - FDLRX) to less than or | |||
equal to 0.92 for re-channeled fuel; and | |||
* the function of the reactor recirculation pump high flow electrical and mechanical | |||
stops (non-safety related) were credited in the analysis. | |||
The inspectors determined that the inadequate design control over fuel rechanneling efforts which resulted in fuel spacer damage at Susquehanna constituted a performance deficiency and a finding. | The inspectors determined that the inadequate design control over fuel rechanneling efforts which resulted in fuel spacer damage at Susquehanna constituted a performance deficiency and a finding. | ||
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=====Enforcement:===== | =====Enforcement:===== | ||
Appendix B of 10 CFR 50, Criterion III, Design Control, states, in part, that: Measures shall be established for the selection and review for the suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of systems, structures and components. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design. Contrary to these requirements, on or before October 20, 2007, PPL installed new fuel channels on exposed fuel bundles, without the effects of differing operating and irradiation exposure histories of the bundle spacers and channels being properly addressed as part of a detailed design review. Because this violation is of very low safety significance and entered into the Corrective Action system (CR 935833), it is being treated as a non-cited violation consistent with section VI.A. of the NRC enforcement policy. (NCV 050000387, 388/2007005-01, Inadequate Design Control to Support Fuel Rechanneling Activities) | Appendix B of 10 CFR 50, Criterion III, Design Control, states, in part, that: Measures shall be established for the selection and review for the suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of systems, structures and components. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design. Contrary to these requirements, on or before October 20, 2007, PPL installed new fuel channels on exposed fuel bundles, without the effects of differing operating and irradiation exposure histories of the bundle spacers and channels being properly addressed as part of a detailed design review. Because this violation is of very low safety significance and entered into the Corrective Action system (CR 935833), it is being treated as a non-cited violation consistent with section VI.A. of the NRC enforcement policy. (NCV 050000387, 388/2007005-01, Inadequate Design Control to Support Fuel Rechanneling Activities) | ||
{{a|1R13}} | {{a|1R13}} | ||
==== | ==1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 6 Samples) a.== | ||
Inspection Scope | |||
The inspectors reviewed the assessment and management of selected maintenance activities to evaluate the effectiveness of PPL's risk management for planned and emergent work. The inspectors compared the risk assessments and risk management actions to the requirements of 10 CFR Part 50.65(a)(4) and the recommendations of NUMARC 93-01, Section 11, "Assessment of Risk Resulting from Performance of Maintenance Activities." The inspectors evaluated the selected activities to determine whether risk assessments were performed when required and appropriate risk management actions were identified. | The inspectors reviewed the assessment and management of selected maintenance activities to evaluate the effectiveness of PPL's risk management for planned and emergent work. The inspectors compared the risk assessments and risk management actions to the requirements of 10 CFR Part 50.65(a)(4) and the recommendations of NUMARC 93-01, Section 11, "Assessment of Risk Resulting from Performance of Maintenance Activities." The inspectors evaluated the selected activities to determine whether risk assessments were performed when required and appropriate risk management actions were identified. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R15}} | No findings of significance were identified. {{a|1R15}} | ||
==1R15 Operability Evaluations (71111.15 - 4 Samples) | |||
==1R15 Operability Evaluations (71111.15 - 4 Samples) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed operability determinations that were selected based on risk insights, to assess the adequacy of the evaluations, the use and control of compensatory measures, and compliance with the TSs. In addition, the inspectors reviewed the selected operability determinations to verify whether the determinations were performed in accordance with NDAP-QA-0703, "Operability Assessments." The inspectors used the TSs, Technical Requirements Manual, Final Safety Analysis Report (FSAR), and associated Design Basis Documents as references during these reviews. | The inspectors reviewed operability determinations that were selected based on risk insights, to assess the adequacy of the evaluations, the use and control of compensatory measures, and compliance with the TSs. In addition, the inspectors reviewed the selected operability determinations to verify whether the determinations were performed in accordance with NDAP-QA-0703, "Operability Assessments." The inspectors used the TSs, Technical Requirements Manual, Final Safety Analysis Report (FSAR), and associated Design Basis Documents as references during these reviews. | ||
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* Unit 1, reactor water cleanup (RWCU) isolation on differential flow during cool down, AR 910150 and 911162; | * Unit 1, reactor water cleanup (RWCU) isolation on differential flow during cool down, AR 910150 and 911162; | ||
* Unit 1, chemistry technician de-energized the Unit 1 containment radiation monitor (CRM) instead of the Unit 2 CRM, CR 918927; and | * Unit 1, chemistry technician de-energized the Unit 1 containment radiation monitor (CRM) instead of the Unit 2 CRM, CR 918927; and | ||
* Unit 1 reactor fuel spacer sections found on the fuel prep machines, AR 935833, Revision 0. | * Unit 1 reactor fuel spacer sections found on the fuel prep machines, AR 935833, | ||
Revision 0. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R19}} | No findings of significance were identified. {{a|1R19}} | ||
==1R19 Post-Maintenance Testing (71111.19 - 5 Samples) | |||
==1R19 Post-Maintenance Testing (71111.19 - 5 Samples) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors observed portions of post-maintenance testing activities in the field to determine whether the tests were performed in accordance with the approved procedures. The inspectors assessed the test adequacy by comparing the test methodology to the scope of maintenance work performed. In addition, the inspectors evaluated acceptance criteria to determine whether the test demonstrated that components satisfied the applicable design and licensing bases and TS requirements. | The inspectors observed portions of post-maintenance testing activities in the field to determine whether the tests were performed in accordance with the approved procedures. The inspectors assessed the test adequacy by comparing the test methodology to the scope of maintenance work performed. In addition, the inspectors evaluated acceptance criteria to determine whether the test demonstrated that components satisfied the applicable design and licensing bases and TS requirements. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R20}} | No findings of significance were identified. {{a|1R20}} | ||
==1R20 Refueling and Other Outage Activities | |||
==1R20 Refueling and Other Outage Activities | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed the outage risk management plan for the Unit 1 outage for fuel assembly rechanneling, conducted from October 12, 2007 to October 29, 2007, to confirm that PPL had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured defense-in-depth barriers. Inspectors observed the reactor shutdown including the control rods which were slow to settle and the associated control rod inoperabilities as described in Event Notification 43722 and Condition Report 918927. During the rechanneling outage, the inspector observed or reviewed the outage activities listed below. | The inspectors reviewed the outage risk management plan for the Unit 1 outage for fuel assembly rechanneling, conducted from October 12, 2007 to October 29, 2007, to confirm that PPL had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured defense-in-depth barriers. Inspectors observed the reactor shutdown including the control rods which were slow to settle and the associated control rod inoperabilities as described in Event Notification 43722 and Condition Report 918927. During the rechanneling outage, the inspector observed or reviewed the outage activities listed below. | ||
* Establishment of a reactor vessel cool down rate; | * Establishment of a reactor vessel cool down rate; | ||
* Establishment of shutdown cooling using the 'A' residual heat removal system; | * Establishment of shutdown cooling using the 'A' residual heat removal system; | ||
* Outage configuration controls including: | * Outage configuration controls including: | ||
1) | |||
1)availability and accuracy of reactor coolant system instrumentation; | |||
2)availability of nuclear instrumentation; | |||
3)electrical power alignments; | |||
4)decay heat removal system operation; | |||
5)availability of reactor inventory makeup water systems; and | |||
6)secondary containment controls and integrity. | |||
* Drywell walkdown after shutdown and prior to final closeout; | * Drywell walkdown after shutdown and prior to final closeout; | ||
* Fuel bundle rechanneling work on the refueling floor; and | * Fuel bundle rechanneling work on the refueling floor; and | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R22}} | No findings of significance were identified. {{a|1R22}} | ||
==1R22 Surveillance Testing (71111.22 - 5 Samples) | |||
==1R22 Surveillance Testing (71111.22 - 5 Samples) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors observed portions of selected surveillance test activities in the control room and in the field and reviewed test data results. The inspectors compared the test results to the established acceptance criteria and the applicable TS or Technical Requirements Manual operability and surveillance requirements to evaluate whether the systems were capable of performing their intended safety functions. The observed or reviewed surveillance tests included: | The inspectors observed portions of selected surveillance test activities in the control room and in the field and reviewed test data results. The inspectors compared the test results to the established acceptance criteria and the applicable TS or Technical Requirements Manual operability and surveillance requirements to evaluate whether the systems were capable of performing their intended safety functions. The observed or reviewed surveillance tests included: | ||
* Unit 1, scram time measurement of control rods, SR-155-004; | * Unit 1, scram time measurement of control rods, SR-155-004; | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R23}} | No findings of significance were identified. {{a|1R23}} | ||
==1R23 Temporary Plant Modifications (71111.23 - 2 Samples) | |||
==1R23 Temporary Plant Modifications (71111.23 - 2 Samples) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed a temporary plant modification to determine whether the temporary change adversely affected system or support system availability, or adversely affected a function important to plant safety. The inspectors reviewed the associated system design bases, including the FSAR, TSs, and assessed the adequacy of the safety determination screenings and evaluations. The inspectors also assessed configuration control of the temporary changes by reviewing selected drawings and procedures to verify that appropriate revisions had been made. The inspectors compared the actual installations to the temporary modification documents to determine whether the implemented changes were consistent with the approved documents. The inspectors reviewed selected post-installation test results to determine whether the actual impact of the temporary changes had been adequately demonstrated by the test. | The inspectors reviewed a temporary plant modification to determine whether the temporary change adversely affected system or support system availability, or adversely affected a function important to plant safety. The inspectors reviewed the associated system design bases, including the FSAR, TSs, and assessed the adequacy of the safety determination screenings and evaluations. The inspectors also assessed configuration control of the temporary changes by reviewing selected drawings and procedures to verify that appropriate revisions had been made. The inspectors compared the actual installations to the temporary modification documents to determine whether the implemented changes were consistent with the approved documents. The inspectors reviewed selected post-installation test results to determine whether the actual impact of the temporary changes had been adequately demonstrated by the test. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
1EP6 Drill Evaluation (71114.06 - 1 Sample) | 1EP6 Drill Evaluation (71114.06 - 1 Sample) | ||
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==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
===Cornerstone: Occupational Radiation Safety=== | ===Cornerstone: Occupational Radiation Safety=== | ||
2OS1 Access Control to Radiologically Significant Areas (71121.01 - 6 Samples) | 2OS1 Access Control to Radiologically Significant Areas (71121.01 - 6 Samples) | ||
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The inspectors reviewed radiological problem reports since the last inspection which found that the cause of the event was due to radiation worker errors. The inspectors determined if there was an observable pattern traceable to a similar cause. The inspectors determined if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. The inspector discussed with the radiation protection manager any problems with the correction actions planned or taken. | The inspectors reviewed radiological problem reports since the last inspection which found that the cause of the event was due to radiation worker errors. The inspectors determined if there was an observable pattern traceable to a similar cause. The inspectors determined if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. The inspector discussed with the radiation protection manager any problems with the correction actions planned or taken. | ||
The inspectors verified adequate posting and locking of entrances to high dose rate - | The inspectors verified adequate posting and locking of entrances to high dose rate - high radiation areas, and very high radiation areas. | ||
high radiation areas, and very high radiation areas. | |||
The inspectors reviewed radiological problem reports since the last inspection that found the cause of the event was radiation protection technician error. The inspectors determined if there was an observable pattern traceable to a similar cause. The inspector determined if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. | The inspectors reviewed radiological problem reports since the last inspection that found the cause of the event was radiation protection technician error. The inspectors determined if there was an observable pattern traceable to a similar cause. The inspector determined if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
2OS2 ALARA Planning and Controls (71121.02 - 3 Samples) | 2OS2 ALARA Planning and Controls (71121.02 - 3 Samples) | ||
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The inspectors reviewed the assumptions and basis for the current annual collective exposure estimate. The inspectors reviewed applicable procedures to determine the methodology for estimating work activity-specific exposures and the intended dose outcome. | The inspectors reviewed the assumptions and basis for the current annual collective exposure estimate. The inspectors reviewed applicable procedures to determine the methodology for estimating work activity-specific exposures and the intended dose outcome. | ||
The inspectors determined if there had been any declared pregnant workers during the current assessment period. The inspectors reviewed the exposure results and monitoring controls employed by the licensee with respect to requirements of 10 CFR 20. | The inspectors determined if there had been any declared pregnant workers during the current assessment period. The inspectors reviewed the exposure results and monitoring controls employed by the licensee with respect to requirements of | ||
10 CFR 20. | |||
The inspectors observed and reviewed outage work activities associated with the Unit 1 fuel rechanneling, radwaste filter work, drywell activities, turbine/condenser valve work and the Control Room Emergency Outside Air Supply System (CREOAS) activities. | The inspectors observed and reviewed outage work activities associated with the Unit 1 fuel rechanneling, radwaste filter work, drywell activities, turbine/condenser valve work and the Control Room Emergency Outside Air Supply System (CREOAS) activities. | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
A self-revealing finding having very low safety significance (Green) was identified due to a deficiency in the area of maintaining occupational radiation exposures as low as is reasonably achievable (ALARA). ALARA and work planning for the CREOAS modification was less than adequate resulting in collective exposure for the work to expand from 3.37 person-rem to 11.9 person-rem. | A self-revealing finding having very low safety significance (Green) was identified due to a deficiency in the area of maintaining occupational radiation exposures as low as is reasonably achievable (ALARA). ALARA and work planning for the CREOAS modification was less than adequate resulting in collective exposure for the work to expand from 3.37 person-rem to 11.9 person-rem. | ||
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Traditional enforcement is not applicable since these matters did not have an actual safety consequence, or the potential for impacting the NRCs ability to perform its regulatory function. As aggregated, these matters are considered more than minor since each issue is comparable to a more than minor ALARA example described in IMC 0612, Appendix E. While no significant exposure was received by any one of the affected workers, the Significance Determination Process applies because the occurrence involved collective dose that resulted from the licensees inability to properly plan and control work during a refueling outage (ALARA planning example of the Program and Process attribute). The finding was determined to be of low safety significance (Green) because it did not involve issues involving access to radiologically significant areas; did not result in, nor was there a substantial potential for, an overexposure; and the licensees ability to assess dose was not compromised. The finding was entered into the licensees corrective action program. The finding is associated with the ALARA planning attribute of the radiation safety cornerstone, and affects the objective of providing adequate protection of the worker from exposure to radiation. | Traditional enforcement is not applicable since these matters did not have an actual safety consequence, or the potential for impacting the NRCs ability to perform its regulatory function. As aggregated, these matters are considered more than minor since each issue is comparable to a more than minor ALARA example described in IMC 0612, Appendix E. While no significant exposure was received by any one of the affected workers, the Significance Determination Process applies because the occurrence involved collective dose that resulted from the licensees inability to properly plan and control work during a refueling outage (ALARA planning example of the Program and Process attribute). The finding was determined to be of low safety significance (Green) because it did not involve issues involving access to radiologically significant areas; did not result in, nor was there a substantial potential for, an overexposure; and the licensees ability to assess dose was not compromised. The finding was entered into the licensees corrective action program. The finding is associated with the ALARA planning attribute of the radiation safety cornerstone, and affects the objective of providing adequate protection of the worker from exposure to radiation. | ||
The ALARA rule contained in 10 CFR 20.1101(b) Statements of Consideration indicates that compliance with the ALARA requirement will be judged on whether the licensee has incorporated measures to track and, if necessary, to reduce exposures and not whether exposures and doses represent an absolute minimum or whether the licensee has used all possible methods to reduce exposures. The overall exposure performance of the nuclear power plant is used to determine compliance with the ALARA rule. Since Susquehanna is below the three-year-rolling-average of 240 person-rem, no violation of regulatory requirements [10CFR20.1101(b)] has occurred. (FIN 05000387/2007005-02, 05000388/2007005-02, Failure to Maintain Occupational Radiation Exposure As Low As Reasonably Achievable During CREOAS Work)2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - 4 Samples) | The ALARA rule contained in 10 CFR 20.1101(b) Statements of Consideration indicates that compliance with the ALARA requirement will be judged on whether the licensee has incorporated measures to track and, if necessary, to reduce exposures and not whether exposures and doses represent an absolute minimum or whether the licensee has used all possible methods to reduce exposures. The overall exposure performance of the nuclear power plant is used to determine compliance with the ALARA rule. Since Susquehanna is below the three-year-rolling-average of 240 person-rem, no violation of regulatory requirements [10CFR20.1101(b)] has occurred. (FIN 05000387/2007005-02, 05000388/2007005-02, Failure to Maintain Occupational Radiation Exposure As Low As Reasonably Achievable During CREOAS Work) | ||
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - 4 Samples) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
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==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
{{a|4OA1}} | {{a|4OA1}} | ||
==4OA1 Performance Indicator Verification (71151 - 19 Samples) | |||
==4OA1 Performance Indicator Verification== | |||
(71151 - 19 Samples) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed PPLs performance indicator (PI) data, for the period of December 2006 through November 2007, to verify whether the PI data was accurate and complete. The inspectors examined selected samples of PI data, PI data summary reports, and plant records. The inspectors compared the PI data against the guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline. The following performance indicators were included in this review: | The inspectors reviewed PPLs performance indicator (PI) data, for the period of December 2006 through November 2007, to verify whether the PI data was accurate and complete. The inspectors examined selected samples of PI data, PI data summary reports, and plant records. The inspectors compared the PI data against the guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline. The following performance indicators were included in this review: | ||
Initiating Event Performance Indicators | Initiating Event Performance Indicators | ||
* Units 1 and 2 scrams with complications. | * Units 1 and 2 scrams with complications. | ||
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===Cornerstone: Physical Protection=== | ===Cornerstone: Physical Protection=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspector performed a review of PI data submitted by the licensee for the Physical Protection Cornerstone. The review was conducted of the licensees programs for gathering, processing, evaluating, and submitting data for the Fitness-for-Duty, Personnel Screening, and Protected Area Security Equipment PIs. The inspector verified that the PIs had been properly reported as specified in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5. The review included the licensees tracking and trending reports, personnel interviews and security event reports for the PI data collected since the last security baseline inspection. The inspector noted from the licensees submittal that there were no reported failures to properly implement the requirements of 10 CFR 73 and 10 CFR 26 during the reporting period. This inspection activity represents the completion of three | The inspector performed a review of PI data submitted by the licensee for the Physical Protection Cornerstone. The review was conducted of the licensees programs for gathering, processing, evaluating, and submitting data for the Fitness-for-Duty, Personnel Screening, and Protected Area Security Equipment PIs. The inspector verified that the PIs had been properly reported as specified in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5. The review included the licensees tracking and trending reports, personnel interviews and security event reports for the PI data collected since the last security baseline inspection. The inspector noted from the licensees submittal that there were no reported failures to properly implement the requirements of 10 CFR 73 and 10 CFR 26 during the reporting period. This inspection activity represents the completion of three | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===Cornerstone: Occupational Radiation Safety (1 Sample)=== | ===Cornerstone: Occupational Radiation Safety (1 Sample)=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed all licensee PIs for the Occupational Exposure Cornerstone for follow-up. The inspectors reviewed a listing of licensee action reports for the period January 1, 2007 through November 26, 2007, for issues related to the occupational radiation safety performance indicator, which measures non-conformances with high radiation areas greater than 1R/hr and unplanned personnel exposures greater than 100 mrem total effective dose equivalent (TEDE), 5 rem skin dose equivalent (SDE),1.5 rem lens dose equivalent (LDE), or 100 mrem to the unborn child. | The inspectors reviewed all licensee PIs for the Occupational Exposure Cornerstone for follow-up. The inspectors reviewed a listing of licensee action reports for the period January 1, 2007 through November 26, 2007, for issues related to the occupational radiation safety performance indicator, which measures non-conformances with high radiation areas greater than 1R/hr and unplanned personnel exposures greater than 100 mrem total effective dose equivalent (TEDE), 5 rem skin dose equivalent (SDE),1.5 rem lens dose equivalent (LDE), or 100 mrem to the unborn child. | ||
| Line 409: | Line 505: | ||
===Cornerstone: Public Radiation Safety (1 Sample)=== | ===Cornerstone: Public Radiation Safety (1 Sample)=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed a listing of licensee action reports for the period January 1, 2007 through November 26, 2007, for issues related to the public radiation safety performance indicator, which measures radiological effluent release occurrences per site that exceed 1.5 mrem/qtr whole body or 5 mrem/qtr organ dose for liquid effluents; or 5 mrads/qtr gamma air dose, 10 mrads/qtr beta air dose; or 7.5 mrems/qtr organ doses from I-131, I-133, H-3 and particulates for gaseous effluents. | The inspectors reviewed a listing of licensee action reports for the period January 1, 2007 through November 26, 2007, for issues related to the public radiation safety performance indicator, which measures radiological effluent release occurrences per site that exceed 1.5 mrem/qtr whole body or 5 mrem/qtr organ dose for liquid effluents; or 5 mrads/qtr gamma air dose, 10 mrads/qtr beta air dose; or 7.5 mrems/qtr organ doses from I-131, I-133, H-3 and particulates for gaseous effluents. | ||
| Line 416: | Line 511: | ||
No findings of significance were identified. | No findings of significance were identified. | ||
{{a|4OA2}} | {{a|4OA2}} | ||
Annual Samples) | ==4OA2 Identification and Resolution of Problems== | ||
(71152 - 1 Semi-Annual Sample and 2 Annual Samples) | |||
===.1 Review of Items Entered into the Corrective Action Program=== | ===.1 Review of Items Entered into the Corrective Action Program=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
As required by Inspection Procedure (IP) 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed screening of all items entered into PPLs corrective action program. This was accomplished by reviewing the description of each new action request/condition report and attending daily management meetings. | As required by Inspection Procedure (IP) 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed screening of all items entered into PPLs corrective action program. This was accomplished by reviewing the description of each new action request/condition report and attending daily management meetings. | ||
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===.2 Semi-Annual Review to Identify Trends=== | ===.2 Semi-Annual Review to Identify Trends=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
As required by IP71152, Identification and Resolution of Problems, the inspectors performed a semi-annual review of PPLs corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. This trend review considered the results of daily inspector corrective action program item screenings discussed in Section 4OA2.1. The review also included issues described in system health reports, corrective maintenance work orders, PPL management meetings, regional inspector exit meetings, and maintenance rule assessments. This review concentrated on the six-month period of July 2007 through December 2007, although some examples were prior to this time period to confirm potential trends. The inspectors compared and contrasted their results with the results in PPLs internal assessment reports and trending. Corrective actions that were initiated in response to inspector observations and the issues identified in PPL trend reports were also reviewed. | As required by IP71152, Identification and Resolution of Problems, the inspectors performed a semi-annual review of PPLs corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. This trend review considered the results of daily inspector corrective action program item screenings discussed in Section 4OA2.1. The review also included issues described in system health reports, corrective maintenance work orders, PPL management meetings, regional inspector exit meetings, and maintenance rule assessments. This review concentrated on the six-month period of July 2007 through December 2007, although some examples were prior to this time period to confirm potential trends. The inspectors compared and contrasted their results with the results in PPLs internal assessment reports and trending. Corrective actions that were initiated in response to inspector observations and the issues identified in PPL trend reports were also reviewed. | ||
| Line 436: | Line 529: | ||
No findings of significance were identified. | No findings of significance were identified. | ||
Procedure Use and Compliance The inspectors identified an adverse trend in the area of procedure use and compliance. | Procedure Use and Compliance | ||
The inspectors identified an adverse trend in the area of procedure use and compliance. | |||
Specifically, inspectors found an increase in the number of minor procedure violations and inspection items with procedure use and compliance contributors during baseline inspection activities. Procedure use issues were observed and documented in the corrective action system for multiple work groups. This identified potential trend was communicated to PPL. | Specifically, inspectors found an increase in the number of minor procedure violations and inspection items with procedure use and compliance contributors during baseline inspection activities. Procedure use issues were observed and documented in the corrective action system for multiple work groups. This identified potential trend was communicated to PPL. | ||
| Line 442: | Line 537: | ||
PPL also identified this potential trend during internal functional group assessments, entered the issue into the corrective action program, and performed a common cause analysis for some of the more recent examples during the last quarter of 2007. | PPL also identified this potential trend during internal functional group assessments, entered the issue into the corrective action program, and performed a common cause analysis for some of the more recent examples during the last quarter of 2007. | ||
As previously documented in Inspection Report 2007-003, PPL issued an internal communication (Hot Box 07-07) on June 29, 2007, to increase worker awareness of the observed trend in human performance issues related to procedural compliance and usage. One of these examples was from inspectors witnessing non-licensed operators aligning the E EDG without utilizing one of the established step-by-step operating procedures. (NCV 2007003-01, PIM #78972) | As previously documented in Inspection Report 2007-003, PPL issued an internal communication (Hot Box 07-07) on June 29, 2007, to increase worker awareness of the observed trend in human performance issues related to procedural compliance and usage. One of these examples was from inspectors witnessing non-licensed operators aligning the E EDG without utilizing one of the established step-by-step operating procedures. (NCV 2007003-01, PIM #78972) | ||
Inspectors identified other instances of procedure use issues in the electrical maintenance, chemistry, operations and engineering departments during the second half of 2007. For example: | Inspectors identified other instances of procedure use issues in the electrical maintenance, chemistry, operations and engineering departments during the second half of 2007. For example: | ||
* In July 2007 after PPL identified reactor building scaffolding that was not built to specifications, inspectors identified additional reactor building scaffolds that were not built according to procedures and standards. | * In July 2007 after PPL identified reactor building scaffolding that was not built to specifications, inspectors identified additional reactor building scaffolds that were not built according to procedures and standards. | ||
* During a December 2007 post-maintenance testing inspection, the inspectors questioned whether equipment operators were observing stabilizer valve flow indications as described by the control rod drive testing procedure. The Control Rod Drive (CRD) system engineer responded that there was an open Action Request to provide clarification to this procedure. The inspectors found that an action request was previously written to document a previous NRC inspectors question on this same issue. | * During a December 2007 post-maintenance testing inspection, the inspectors questioned whether equipment operators were observing stabilizer valve flow indications as described by the control rod drive testing procedure. The Control Rod Drive (CRD) system engineer responded that there was an open Action Request to provide clarification to this procedure. The inspectors found that an action request was previously written to document a previous NRC inspectors question on this same issue. | ||
* During a NRC Performance Indicator (PI) inspection, the inspectors identified that PI records were not retained or readily retrievable as required by PPL procedures. Although a performance issue, the inspectors determined that the required information was sufficient to support the inspection | * During a NRC Performance Indicator (PI) inspection, the inspectors identified that PI records were not retained or readily retrievable as required by PPL procedures. Although a performance issue, the inspectors determined that the required information was sufficient to support the inspection | ||
Increase in Control Room Alarm Panel Condition Reports and Emergent Work Inspectors identified a potential adverse trend in control room alarm panel performance. | PPL also identified human performance procedure related issues through the 3rd quarter 2007 Operations department functional unit excellence plan (AR 908670). The inspectors also determined that some of the procedure use and adherence issues observed during the 4th quarter were administrative or documentation related, and none of the individual issues were found to be of more than minor significance. | ||
Increase in Control Room Alarm Panel Condition Reports and Emergent Work | |||
Inspectors identified a potential adverse trend in control room alarm panel performance. | |||
The adverse trend challenges the operations staff by making it more difficult to assess plant parameters and system performance. When alarm system power supplies failed, operators were increasing their monitoring of local field panels to compensate for the associated control room alarms for that system or train being inoperable. The number of plant annunciator system condition reports is considered to be on an increasing trend. | The adverse trend challenges the operations staff by making it more difficult to assess plant parameters and system performance. When alarm system power supplies failed, operators were increasing their monitoring of local field panels to compensate for the associated control room alarms for that system or train being inoperable. The number of plant annunciator system condition reports is considered to be on an increasing trend. | ||
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This PI&R trend review documents the identified adverse trend in procedure use and adherence as well as a potential adverse trend in control room annunicator system performance at Susquehanna. These observations were not more-than-minor performance deficiencies that affected any safety cornerstone during the inspection period. Inspector observations were communicated to PPL at weekly management meetings and the quarterly exit meeting. | This PI&R trend review documents the identified adverse trend in procedure use and adherence as well as a potential adverse trend in control room annunicator system performance at Susquehanna. These observations were not more-than-minor performance deficiencies that affected any safety cornerstone during the inspection period. Inspector observations were communicated to PPL at weekly management meetings and the quarterly exit meeting. | ||
===.3 Human Performance - Work Control, Work Package Quality and Supervisory Oversight | ===.3 Human Performance=== | ||
- Work Control, Work Package Quality and Supervisory Oversight (1 Annual Sample) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
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No findings of significance were identified. | No findings of significance were identified. | ||
Assessment - Control of Station Work, Work Package Quality, & Supervisory Oversight The inspectors determined that PPL is engaging significant effort across the station with respect to control of work, work package quality, and supervisory oversight. Many corrective actions have been taken to address the deficiencies, and several corrective actions are currently ongoing. The Maintenance Department has led the corrective action effort, through the hiring of an independent contractor to perform coaching and training in human performance, focusing their effort on supervisory oversight. Inspectors observed that maintenance supervisors are being trained on the importance of implementing several standards, including in-field walkdowns and observations, procedural use and adherence, work package review, and coaching to change behavior. | Assessment - Control of Station Work, Work Package Quality, & Supervisory Oversight | ||
The inspectors determined that PPL is engaging significant effort across the station with respect to control of work, work package quality, and supervisory oversight. Many corrective actions have been taken to address the deficiencies, and several corrective actions are currently ongoing. The Maintenance Department has led the corrective action effort, through the hiring of an independent contractor to perform coaching and training in human performance, focusing their effort on supervisory oversight. Inspectors observed that maintenance supervisors are being trained on the importance of implementing several standards, including in-field walkdowns and observations, procedural use and adherence, work package review, and coaching to change behavior. | |||
The independent contractor training and coaching was also implemented within the Work Planning Department. Additional corrective actions in the area of work package quality include actions to improve procedure quality and assigning additional personnel to support procedure writing. | The independent contractor training and coaching was also implemented within the Work Planning Department. Additional corrective actions in the area of work package quality include actions to improve procedure quality and assigning additional personnel to support procedure writing. | ||
| Line 478: | Line 579: | ||
Since procedure use and adherence is a specific human error barrier, inspectors performed an additional PI&R annual sample on Procedure Use and Adherence during the last quarter of 2007. Inspector review of this assessment found that PPL identified similar results and trends when compared to results of previously performed assessments in the areas of work control and supervisory oversight, as mentioned above. The inspectors observed no current plan in place for PPL to integrate the results and planned corrective actions from the recent station assessment on use of human performance tools with assessments performed in the areas of work control, work package quality, and supervisory oversight. | Since procedure use and adherence is a specific human error barrier, inspectors performed an additional PI&R annual sample on Procedure Use and Adherence during the last quarter of 2007. Inspector review of this assessment found that PPL identified similar results and trends when compared to results of previously performed assessments in the areas of work control and supervisory oversight, as mentioned above. The inspectors observed no current plan in place for PPL to integrate the results and planned corrective actions from the recent station assessment on use of human performance tools with assessments performed in the areas of work control, work package quality, and supervisory oversight. | ||
===.4 Human Performance - Procedural Use and Adherence (1 Annual Sample) | ===.4 Human Performance - Procedural Use and Adherence=== | ||
(1 Annual Sample) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
| Line 488: | Line 590: | ||
No findings of significance were identified. | No findings of significance were identified. | ||
Assessment - Human Performance - Procedural Use and Adherence One issue identified on November 26, 2007, was an open jumper test switch found in Upper Relay Room Panel 1C621 which was not removed following previous RCIC system and logic functional testing performed in October 2007. Inspectors reviewed PPLs corrective actions including cause analysis, extent of condition, and timeliness of corrective actions. Inspectors found that PPL utilized a Level 2 Cause evaluation in the corrective action system and that PPL conducted Event and Accountability Review Boards in early December. Inspectors observed a detailed review of extent of condition and apparent causes associated with the issue. This human performance issue and corrective actions will also be reviewed by the PPL Corrective Action Review Board. | Assessment - Human Performance - Procedural Use and Adherence | ||
One issue identified on November 26, 2007, was an open jumper test switch found in Upper Relay Room Panel 1C621 which was not removed following previous RCIC system and logic functional testing performed in October 2007. Inspectors reviewed PPLs corrective actions including cause analysis, extent of condition, and timeliness of corrective actions. Inspectors found that PPL utilized a Level 2 Cause evaluation in the corrective action system and that PPL conducted Event and Accountability Review Boards in early December. Inspectors observed a detailed review of extent of condition and apparent causes associated with the issue. This human performance issue and corrective actions will also be reviewed by the PPL Corrective Action Review Board. | |||
Although no effectiveness review was conducted for this specific issue, PPL initiated a common cause evaluation for engineering testing errors that have occurred in 2007. | Although no effectiveness review was conducted for this specific issue, PPL initiated a common cause evaluation for engineering testing errors that have occurred in 2007. | ||
| Line 502: | Line 606: | ||
Although each case of a procedure non-compliance mentioned in this PI&R assessment was determined to be a performance issue, the inspectors determined that the issues were licensee-identified, had been placed in the corrective action program, and were not of more-than-minor significance. One exception, however, was a licensee-identified procedure violation that did negatively affect safety cornerstone objectives regarding unqualified seismic material left in the Unit 1 residual heat removal pump room. | Although each case of a procedure non-compliance mentioned in this PI&R assessment was determined to be a performance issue, the inspectors determined that the issues were licensee-identified, had been placed in the corrective action program, and were not of more-than-minor significance. One exception, however, was a licensee-identified procedure violation that did negatively affect safety cornerstone objectives regarding unqualified seismic material left in the Unit 1 residual heat removal pump room. | ||
Overall Assessment for PI&R Annual Samples The inspectors determined that PPL is appropriately identifying problems in the areas of human performance - specifically, work control, work package quality, supervisory oversight, as well as, procedure use and adherence. Characterization and evaluation of the problems is generally appropriate, though inspectors observed no current plan for PPL to integrate the results and planned corrective actions from the recent station assessment on use of human performance tools with the independent assessments performed in the areas of work control, work package quality, and supervisory oversight. | Overall Assessment for PI&R Annual Samples | ||
The inspectors determined that PPL is appropriately identifying problems in the areas of human performance - specifically, work control, work package quality, supervisory oversight, as well as, procedure use and adherence. Characterization and evaluation of the problems is generally appropriate, though inspectors observed no current plan for PPL to integrate the results and planned corrective actions from the recent station assessment on use of human performance tools with the independent assessments performed in the areas of work control, work package quality, and supervisory oversight. | |||
Procedure use and adherence appears to be on a negative trend as compared to the other human performance barriers and tools which do not show the same adverse or negative trend. Inspectors have determined corrective actions taken to address the issues thus far have been appropriate, however, several corrective actions are currently ongoing and the inspectors will continue to monitor station performance. | Procedure use and adherence appears to be on a negative trend as compared to the other human performance barriers and tools which do not show the same adverse or negative trend. Inspectors have determined corrective actions taken to address the issues thus far have been appropriate, however, several corrective actions are currently ongoing and the inspectors will continue to monitor station performance. | ||
{{a|4OA6}} | {{a|4OA6}} | ||
==4OA6 Meetings, Including Exit== | ==4OA6 Meetings, Including Exit== | ||
On January 17, 2007, the inspectors presented their findings to Mr. C. Gannon, Vice President - Nuclear Operations, and other members of his staff, who acknowledged the findings. | On January 17, 2007, the inspectors presented their findings to Mr. C. Gannon, Vice President - Nuclear Operations, and other members of his staff, who acknowledged the findings. | ||
{{a|4OA7}} | {{a|4OA7}} | ||
==4OA7 Licensee-Identified Violations== | ==4OA7 Licensee-Identified Violations== | ||
The following violation of very low safety significance (Green) was identified by PPL and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited Violation. | The following violation of very low safety significance (Green) was identified by PPL and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited Violation. | ||
| Line 523: | Line 629: | ||
==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
===Licensee Personnel=== | ===Licensee Personnel=== | ||
: [[contact::R. Bogar]], EDG System Engineer | : [[contact::R. Bogar]], EDG System Engineer | ||
: [[contact::D. Brophy]], Acting Regulatory Affairs Supervisor | : [[contact::D. Brophy]], Acting Regulatory Affairs Supervisor | ||
: [[contact::P. Capotosto]], Supervising Engineer, Electrical Engineering | : [[contact::P. Capotosto]], Supervising Engineer, Electrical Engineering | ||
: [[contact::D. DAngelo]], Manager Station Engineering | : [[contact::D. DAngelo]], Manager Station Engineering | ||
: [[contact::S. Davis]], Senior Engineer, Programs and Components | : [[contact::S. Davis]], Senior Engineer, Programs and Components | ||
: [[contact::J. Helsel]], Manager Nuclear Operations | : [[contact::J. Helsel]], Manager Nuclear Operations | ||
: [[contact::C. Hoffman]], Manager, Nuclear Fuels | : [[contact::C. Hoffman]], Manager, Nuclear Fuels | ||
: [[contact::J. Jeanguenat]], ESW System Engineer | : [[contact::J. Jeanguenat]], ESW System Engineer | ||
: [[contact::W. Kahler]], Senior Engineer, Nuclear Fuels | : [[contact::W. Kahler]], Senior Engineer, Nuclear Fuels | ||
: [[contact::R. Kessler]], Senior Health Physicist - ALARA | : [[contact::R. Kessler]], Senior Health Physicist - ALARA | ||
: [[contact::G. Machalick]], Senior Engineer, Programs and Components | : [[contact::G. Machalick]], Senior Engineer, Programs and Components | ||
: [[contact::F. Negvesky]], Senior Engineer | : [[contact::F. Negvesky]], Senior Engineer | ||
: [[contact::J. Pacioti]], Security Operations Coordinator | : [[contact::J. Pacioti]], Security Operations Coordinator | ||
: [[contact::M. Rose]], QA Manager | : [[contact::M. Rose]], QA Manager | ||
: [[contact::V. Schuman]], Radiological Protection Manager | : [[contact::V. Schuman]], Radiological Protection Manager | ||
: [[contact::M. Sleigh]], Security Manager | : [[contact::M. Sleigh]], Security Manager | ||
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED== | ==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED== | ||
===Opened=== | |||
None. | |||
===Opened/Closed=== | |||
: 05000387, 388/2007005-01 NCV Inadequate Design Control to | |||
Support Fuel Rechanneling Activities (Section IR12) | |||
: 05000387, 388/2007005-02 FIN Failure to Maintain Occupational Radiation | |||
Exposure As Low As Reasonably | |||
Achievable During CREOAS Work (Section 2OS2) | |||
===Closed=== | ===Closed=== | ||
BASELINE INSPECTION PROCEDURE PERFORMED | |||
7112101 Access Control | |||
2OS1 7112102 ALARA Planning and Controls | |||
2OS2 7112103 Radiation Monitoring Instrumentation | |||
2OS3 71151 Performance Indicator Verification | |||
4OA1 | |||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} | ||
Latest revision as of 18:04, 14 January 2025
| ML080450365 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 02/14/2008 |
| From: | Paul Krohn Reactor Projects Region 1 Branch 4 |
| To: | Mckinney B Susquehanna |
| KROHN, PG | |
| References | |
| IR-07-005 | |
| Download: ML080450365 (37) | |
Text
February 14, 2008
SUBJECT:
SUSQUEHANNA STEAM ELECTRIC STATION - NRC INTEGRATED INSPECTION REPORT 05000387/2007005 AND 05000388/2007005
Dear Mr. McKinney:
On December 31, 2007, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Susquehanna Steam Electric Station Units 1 and 2. The enclosed integrated inspection report presents the inspection results, which were discussed on January 17, 2008, with you and other members of your staff.
This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
This report documents two NRC-identified findings of very low safety significance (Green). One of these findings was determined to involve violations of NRC requirements. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs), consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Susquehanna Steam Electric Station. In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Paul G. Krohn, Chief Projects Branch 4 Division of Reactor Projects
Docket Nos.
50-387; 50-388 License Nos. NPF-14, NPF-22
Enclosures:
Inspection Report 05000387/2007005 and 05000388/2007005
Attachment: Supplemental Information
REGION I==
Docket No:
50-387, 50-388
License No:
Report No:
05000387/2007005 and 05000388/2007005
Licensee:
Facility:
Susquehanna Steam Electric Station, Units 1 and 2
Location:
Berwick, Pennsylvania
Dates:
October 1, 2007 through December 31, 2007
Inspectors:
F. Jaxheimer, Senior Resident Inspector
S. Hansell, Limerick Senior Resident Inspector P. Finney, Resident Inspector
J. Kulp, Reactor Engineer
T. OHara, Reactor Engineer
J. Furia, Senior Health Physicist
A. Ziedonis, Reactor Inspector
Approved By:
Paul G. Krohn, Chief
Projects Branch 4
Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000387/2007005, 05000388/2007005; 10/01/2007 - 12/31/2007; Susquehanna Steam
Electric Station, Units 1 and 2; Maintenance Effectiveness and ALARA Planning and Controls.
The report covered a 3-month period of inspection by resident inspectors, and announced inspections by regional reactor inspectors and a senior health physicist. Two, Green non-cited violations (NCVs) were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversignt Process, Revision 4, dated December 2006.
NRC-Identified and Self-Revealing Findings
Cornerstone: Barrier Integrity
- Green.
A self-revealing non-cited violation of 10CFR 50 Appendix B, Criterion III,
Design Control, was identified on December 6, 2007, when PPL maintenance personnel found broken pieces of fuel spacer grid assemblies at fuel preparation machines. The damage to fuel assembly spacer assemblies was determined to be from rechanneling activities performed on or before October 20, 2007. The cause of the damaged fuel assemblies was due to the differing exposure histories of fuel channels and fuel bundle spacers not having been adequately analyzed prior to performance of the fuel rechanneling activities. Inspectors determined that the engineering analysis which implemented the allowable applied force limit used in fuel rechanneling procedures had not verified design interfaces, and did not verify the adequacy of design limits. PPL determined that the extent of condition was limited to those rechanneled fuel assemblies re-installed in the Unit 1 or Unit 2 reactors with greater than 25 GigaWatt-Days per Metric Tonne Uranium (GWD/MTU) average exposure.
This finding was more than minor because the finding is related to the Design Control and Human Performance attributes of the barrier integrity cornerstone and negatively impacts the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding) protect the public from radio nuclide releases caused by accidents or events. The inspectors completed a Phase 1 significance determination using IMC 0609 Appendix A, Significance Determination Process Phase 1 screening worksheet, and determined the finding to be of Very Low Safety Significance (Green) because the performance issue only degraded the Fuel Cladding Barrier and its associated cornerstone.
This finding is related to a cross-cutting component in the area of Human Performance associated with work practices H.4.(c) because PPL did not ensure supervisory and management oversight of specific work activities, specifically design reviews which supported the fuel rechanneling procedures used from October 2005 through October 2007 and the collective evaluation of 25 condition reports related to rechanneling difficulties. PPL entered this issue into the corrective action program and promptly initiated compensatory measures to impose fuel thermal limit penalties to assure fuel barrier integrity during reactor operation. (IR12)
Cornerstone: Occupational Radiation Safety
- Green.
A self-revealing finding having very low safety significance was identified due to a deficiency in the area of maintaining occupational radiation exposures as low as is reasonably achievable (ALARA). ALARA and work planning for the control room emergency outside air supply system (CREOAS) modification was less than adequate resulting in collective exposure for the work to expand from 3.37 person-rem to 11.9 person-rem.
The performance deficiency that resulted in the exposure overrun was due to significantly increased hours beyond that planned to perform the work. The root cause of the overrun was determined to be: (1) a failure to include contractor work hours in the ALARA planning process; and (2) design errors which did not properly identify bolting locations for the duct work, requiring extensive on-site rework. Susquehannas three-year rolling average is 101 Person-rem, which is below the SDP criteria of 240 person-rem for Boiling Water Reactors (BWRs), therefore, overall ALARA performance has been effective and this finding is of very low safety significance.
A contributing cause of this finding was related to the Work Control aspect of the Human Performance cross-cutting area because the licensee did not appropriately coordinate work activities by incorporating actions to address the impact of the work on different job activities, and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure plant and human performance. (H.3b)
(Section 2OS2)
Licensee Identified Violations
Violations of very low safety significance, which were identified by PPL have been reviewed by the inspectors. Corrective actions taken or planned by PPL have been entered into PPL's corrective action program. These violations and corrective actions tracking numbers are listed in Section 4OA7 of this report.
REPORT DETAILS
Summary of Plant Status
Susquehanna Steam Electric Station (SSES) Unit 1 began the inspection period at full rated thermal power. The Unit 1 reactor was shutdown on October 12, 2007, for a maintenance and fuel assembly rechanneling outage. The unit was restarted on October 29, 2007, and reached full power operation on November 2, 2007. With the exception of brief power reductions to perform control rod pattern adjustments the unit operated at full power for the remainder of the inspection period.
Unit 2 began the inspection period with the reactor at full rated thermal power and with the exception of brief power reductions to perform control rod pattern adjustments, the reactor operated at full rated power for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
==1R01 Adverse Weather Protection (71111.01 - 2 Samples)
==
.1 Adverse Weather - Readiness for Seasonal Susceptibilities
a. Inspection Scope
During the week of November 8, 2007, the inspectors reviewed system operations during extreme cold weather. Plant walkdowns for selected structures, systems, and components (SSCs) were performed to determine the adequacy of PPLs weather protection features. Inspectors reviewed operator actions to address failures of equipment due to freezing and compensatory actions during adverse cold weather conditions. The inspectors also reviewed and evaluated plant conditions resulting from cold weather and reviewed considerations in PPLs Maintenance Rule station risk assessment. Additional documents that were reviewed are listed in the attachment.
The readiness of the following system was reviewed.
- Units 1 and 2, cold weather preparation, ultimate heat sink systems.
b. Findings
No findings of significance were identified.
.2 Adverse Weather - Impending Adverse Weather Conditions
a. Inspection Scope
On December 15, 2007, during the onset of a snow and ice storm with high winds, the inspectors reviewed PPLs preparations/protection for selected risk significant SSCs exposed to the adverse outdoor conditions. The inspection focused on verifying the design features and implementation of PPLs procedures to protect the mitigating systems from adverse weather effects such that the SSCs remained operable. This included review of open work items on heat trace and other freeze protection measures, plant walkdowns of the selected SSCs, and reviews of the Final Safety Analysis Report (FSAR), Technical Specifications (TS), and plant documents for the selected SSCs. The following outdoor systems were reviewed: condensate storage tanks, fire system valves, emergency safeguards, 4KV transformers, station blackout, diesel and offsite power transformers T-10 and T-20.
b. Findings
No findings of significance were identified.
==1R04 Equipment Alignment (71111.04 - 4 Samples)
==
.1 Partial Walkdown
a. Inspection Scope
The inspectors performed partial walkdowns to verify system and component alignment and to identify any discrepancies that would impact system operability. The inspectors verified that selected portions of redundant or backup systems or trains were available while certain system components were out of service. The inspectors reviewed selected valve positions, electrical power availability, and the general condition of major system components. The walkdowns included the following systems:
- Unit 1, RHR Division I during a Division II scheduled outage window;
- Unit 2, control rod drive system during hydraulic control unit maintenance; and
- Units 1 and 2, high pressure coolant injection (HPCI) heat tracing during testing.
.2 Complete Walkdown
a. Inspection Scope
The inspectors conducted a detailed review of the alignment and condition of the Unit 1 Reactor Core Isolation Cooling System (RCIC). The inspectors reviewed operator rounds, check-off lists, system operating procedures, and system piping and instrumentation diagrams. The inspectors evaluated ongoing maintenance and outstanding condition reports associated with the RCIC system to determine the effect on system health and reliability. The walkdown included the following system:
- Unit 1, reactor core isolation cooling.
b. Findings
No findings of significance were identified.
==1R05 Fire Protection (71111.05 - 9 Samples)
==
.1 Fire Protection - Tours
a. Inspection Scope
The inspectors reviewed PPLs fire protection program to evaluate the required fire protection design features, fire area boundaries, and combustible loading requirements for selected areas. The inspectors walked down those areas to assess PPLs control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures to assess PPL's fire protection program in those areas. The inspected areas included:
- Unit 1, upper relay room, elevation 754, fire zone 0-27E (C-501) area 12, during halon impairment;
- Unit 1, main condenser bay, elevation 656, fire zone 1-31D;
- Unit 1, reactor core isolation cooling room, elevation 645, fire zone 1-D;
- Unit 1, high pressure coolant injection room, elevation 645, fire zone 1-1C;
- Unit 2, lower relay room, elevation 698, fire zone 0-24G, elevation 6980 (C-201)area 21;
- Unit 2, equipment and battery rooms, control structure, elevation 771, fire zones 0-28A-1, 0-28 F, D, T, G, E, C, 0-28 A-1;
- Unit 2, upper relay room, fire zone 0-27A, elevation 7540 (C-502) area 21;
- Unit 2, upper cable spreading room, fire zone 27B, elevation 7540 (C-507), area 21; and
- Unit 2, lower cable spreading room, fire zone 0-25A, elevation 7140 (C-301),area 21.
b. Findings
No findings of significance were identified.
==1R06 Flood Protection Measures (71111.06 - 1 Sample)
==
.1 Internal Flooding
a. Inspection Scope
The inspectors reviewed documents, interviewed plant personnel, and walked down SSCs to evaluate the adequacy of PPLs internal flood protection measures. The inspection focused on verifying that PPLs flooding mitigation plans and equipment were consistent with the design requirements and risk analysis assumptions. The material condition of credited components such as watertight plugs, floor drains, flood detection equipment and alarms were also assessed to determine whether the components were capable of performing their intended function. The inspectors also verified that adequate procedures were in place to identify and respond to floods. The following risk significant area was reviewed:
- Unit 2, high pressure coolant injection (HPCI) room
b. Findings
No findings of significance were identified.
==1R07 Heat Sink Performance (71111.07A - 1 Sample)
a. Inspection Scope
==
The inspectors reviewed PPLs programs for maintenance, testing, and monitoring of risk significant heat exchangers (HXs) to determine whether potential HX deficiencies could mask degraded performance, and to assess the capability of the HXs to perform their design functions. The inspectors assessed whether Susquehannas HX programs conformed to PPLs commitments to NRC Generic Letter 89-13, "Service Water (SW)
System Problems Affecting Safety-Related Equipment." In addition, the inspectors evaluated whether any potential common cause heat sink performance problems could affect multiple HXs in mitigating systems or result in an initiating event. Based on risk significance and prior inspection history, the following HXs were selected:
C Unit 1, reactor core isolation cooling (RCIC) system lube oil cooler, IE21.
The inspectors assessed the external condition of the HXs in the field; reviewed the most recent eddy current data results; inspection and cleaning work results; and reviewed the applicable system heath reports to confirm that results were acceptable and that design basis assumptions for flow rate, plugged tube percentage, and heat transfer capability had been met.
Inspectors reviewed the chemical treatment programs for the spray pond (emergency service water (ESW) ultimate heat sink) and the cooling tower basin (SW heat sink) to verify that potential bio-fouling mechanisms were being addressed, including on-going treatment and monitoring as specified in the chemistry manual. The review included discussions with chemistry personnel and the ESW and SW system engineer.
The inspectors reviewed a sample of condition reports (CRs) related to the selected HXs and SW system, to verify that PPL was appropriately identifying, characterizing, and correcting problems related to these systems and components. Documents reviewed during the inspection are listed in the Attachment.
b. Findings
No findings of significance were identified
==1R11 Licensed Operator Requalification Program (71111.11 - 1 Sample)
a. Inspection Scope
==
On December 21, 2007, the inspectors observed licensed operator simulator training during routine operator requalification training. The inspectors compared their observations to TSs, emergency plan implementation, and the use of system operating procedures. The inspectors also evaluated PPLs critique of the operators' performance to identify discrepancies and deficiencies in operator training. The following training was observed:
C An operating crew simulator scenario that included a simulated failure of the reactor to scram, trip of both control rod drive pumps, trip of the A standby liquid control pump, and the inadvertent closure of the main steam isolation valves.
The scenario included the proper emergency plan Site Area Emergency event classification.
b. Findings
No findings of significance were identified.
==1R12 Maintenance Effectiveness (71111.12 - 1 Sample)
a. Inspection Scope
==
The inspectors evaluated PPLs work practices and follow-up corrective actions for selected SSC issues to assess the effectiveness of PPL's maintenance activities. The inspectors reviewed the performance history of those SSCs and assessed PPLs extent of condition determinations for these issues with potential common cause or generic implications to evaluate the adequacy of PPLs corrective actions. The inspectors reviewed PPL's problem identification and resolution actions for these issues to evaluate whether PPL had appropriately monitored, evaluated, and dispositioned the issues in accordance with PPL procedures and the requirements of 10 CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance." In addition, the inspectors reviewed selected SSC classification, performance criteria and goals, and PPL's corrective actions that were taken or planned, to verify whether the actions were reasonable and appropriate. This review included the associated system design basis, including the Final Safety Analysis Report (FSAR), the Core Operating Limits Report, and previous documented issues with fuel rechanneling activities. In addition, the inspectors performed field walkdowns and interviewed PPL staff to verify whether the identified actions were appropriate to correct the extent of condition for identified performance issues. The following issue was reviewed:
- Units 1 and 2, rechanneling of fuel assemblies; maintenance procedures and effectiveness of quality controls.
b. Findings
Introduction:
A Green self-revealing NCV of 10 CFR Appendix B, Criterion III, Design Control, was identified on December 6, 2007, when PPL maintenance personnel working on the refuel floor identified foreign material at a fuel preparation machine. The foreign material was visually identified to be the outer portions of fuel spacer grid assemblies. As part of the extent of condition investigation, additional spacer grid pieces were found at two other fuel preparation machines within the spent fuel pool (SFP). This failure of plant equipment was promptly entered into the PPL corrective action program and determined to be a Significant Condition Adverse to Quality.
Description:
On December 6, 2007, PPL retrieved the identified fuel spacer pieces from three fuel preparation machines and placed them in a container within the SFP. As part of the investigation into this failure of plant equipment, fuel assembly F21-694 was inspected on December 8, 2007. When de-channeling fuel assembly F21-694 similar debris was observed falling from the fuel assembly after the channel was raised above the lowest spacer position. PPL visually verified that the debris was not from the lowest spacer and, therefore, concluded that the spacer pieces came from a higher axial location on this fuel bundle. Due to lack of foreign material exclusion (FME) controls to capture additional debris, the channel was re-seated on the fuel assembly and inspection of this assembly was suspended. PPL selected a set of 10 additional fuel assemblies that were expected to provide information regarding extent of condition.
PPL could not de-channel two of these fuel assemblies and the additional inspections of eight of these fuel assemblies found no additional spacer debris and found no damaged spacer locations to correspond with the broken spacer pieces retrieved from the fuel preparation machines.
The PPL root cause team identified that the fuel spacer material was most likely from rechanneling activities performed during the Unit 1 October 2007 fuel rechanneling outage. Since no fuel spacer damage sites were located, PPL was unable to visually confirm the identity or the number of fuel assemblies with spacer damage. The rechanneling activities which damaged fuel spacers occurred on or before October 20, 2007, and the fuel spacer pieces were discovered on December 6, 2007, which was greater than or equal to 47 days after the fuel spacers were damaged during a maintenance activity.
Following a review of procedure controls and interviews with PPL staff, inspectors concluded that the engineering analysis which supported the implemented design control measures in the fuel rechanneling procedures (Procedure OP-ORF-007) had not verified design interfaces, and did not verify the adequacy of design limits. This characterization of the performance issue aligns with PPLs identified root cause of an analysis deficiency (calculations: stress, hydraulic, thermal, electrical, other). PPL determined that a design deficiency allowed a rechanneling force limit of 250 pounds, even though applying that amount of force could damage a fuel spacer when there is interference with a fuel channel. The PPL root cause stated that prior to installing new channels on exposed fuel bundles, the effect of differing exposure histories of the channels and fuel bundle spacers had not been adequately analyzed.
Based on the rate of spacer growth as a function of fuel burn-up, PPL determined that the extent of condition was limited to those fuel assemblies rechanneled and reinstalled in Unit 1 and Unit 2 reactors with greater than 25 GWD/MWT average exposure. As such, the missing or damaged spacer plates, which assure turbulent flow between the outer fuel pins and the inner wall of the fuel channel, were evaluated with regard to the impact on linear heat generation rate (LHGR) and critical power performance of the fuel which is installed in both the Unit 1 and Unit 2 reactors. Since a fuel assembly is required to not fail during normal operation and anticipated operational occurrences, the damaged fuel spacer plates caused the core thermal operating limits to be in question.
Based on all the information available, PPL implemented the following three compensatory measures to assure fuel barrier integrity:
- a fuel thermal limit penalty was applied which reduced the maximum fraction of limiting critical power ratio (MFLCPR) to less than or equal to 0.84 for rechanneled fuel;
- a fuel thermal limit penalty was applied which reduced the ratio of the maximum
linear heat generation rate (fraction design limit ratio - FDLRX) to less than or
equal to 0.92 for re-channeled fuel; and
- the function of the reactor recirculation pump high flow electrical and mechanical
stops (non-safety related) were credited in the analysis.
The inspectors determined that the inadequate design control over fuel rechanneling efforts which resulted in fuel spacer damage at Susquehanna constituted a performance deficiency and a finding.
Analysis:
This finding was more than more in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, because the finding is related to the Design Control and Human Performance attributes of the barrier integrity cornerstone and negatively impacts the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding) protect the public from radio nuclide releases caused by accidents or events.
The inspectors completed a Phase 1 significance determination using IMC 0609, Significance Determination Process, using IMC 0609 Appendix A, SDP Phase 1 screening worksheet. The inspectors determined the finding to be of very low safety significance (Green) because the performance issue only degraded the fuel cladding barrier and its associated cornerstone.
Regarding design reviews, PPL was aware of the potential for fuel bundle spacer interferences with fuel channels and implemented procedure changes to address rechanneling difficulties and provide controls on the amount of force applied during rechanneling activities. Inspectors found that the original vendor engineering source document for the 250 pound force limit utilized during rechanneling was based on an design limit of 500 pounds for a spacer side plate (no design reference provided) and this value was divided by 2 to address possible embrittlement and loss of strength due to irradiation (fuel burnup or exposure) without a detailed evaluation of the suitability of this factor for the specific conditions at Susquehanna. The design margin between the maintenance limit and the actual design limit was not determined during the design review process. PPLs acceptance of the fuel vendors force limit without a site specific evaluation as the engineering basis was a missed opportunity to verify that design reviews and design control measures were adequate for the rechanneling of fuel at Susquehanna.
In addition, there were ten corrective action items initiated during the rechanneling activities in 2005 and 2006 related to difficulties in removing or installing fuel channels from fuel and an additional fifteen condition reports written during the Unit 1 October 2007 outage that documented fuel bundles that could not be rechanneled. This corrective action history provided an opportunity for management to revisit actual design margins and initiate some additional measures to assure significant conditions adverse to quality, associated with the rechanneling effort would be promptly identified.
Enforcement:
Appendix B of 10 CFR 50, Criterion III, Design Control, states, in part, that: Measures shall be established for the selection and review for the suitability of application of materials, parts, equipment, and processes that are essential to the safety-related functions of systems, structures and components. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design. Contrary to these requirements, on or before October 20, 2007, PPL installed new fuel channels on exposed fuel bundles, without the effects of differing operating and irradiation exposure histories of the bundle spacers and channels being properly addressed as part of a detailed design review. Because this violation is of very low safety significance and entered into the Corrective Action system (CR 935833), it is being treated as a non-cited violation consistent with section VI.A. of the NRC enforcement policy. (NCV 050000387, 388/2007005-01, Inadequate Design Control to Support Fuel Rechanneling Activities)
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 6 Samples) a.
Inspection Scope
The inspectors reviewed the assessment and management of selected maintenance activities to evaluate the effectiveness of PPL's risk management for planned and emergent work. The inspectors compared the risk assessments and risk management actions to the requirements of 10 CFR Part 50.65(a)(4) and the recommendations of NUMARC 93-01, Section 11, "Assessment of Risk Resulting from Performance of Maintenance Activities." The inspectors evaluated the selected activities to determine whether risk assessments were performed when required and appropriate risk management actions were identified.
The inspectors reviewed scheduled and emergent work activities with licensed operators and work-coordination personnel to evaluate whether risk management action threshold levels were correctly identified. In addition, the inspectors compared the assessed risk configuration to the actual plant conditions and any in-progress evolutions or external events to evaluate whether the assessment was accurate, complete, and appropriate for the emergent work activities. The inspectors performed control room and field walkdowns to verify whether the compensatory measures identified by the risk assessments were appropriately performed. The selected maintenance activities included:
- Unit 1, source range monitor upscale/inoperable and rod block alarm did not prevent rod motion during mode 5 (core alterations), CR 914006;
- Unit 1, equipment-out-of-service risk calculation for C RHR pump, B soluable liquid boron control injection valve and E EDG unavailable;
- Unit 1 standby liquid control (SLC) heat trace turned off on the A SLC pump suction pipe;
- Unit 1, fuel spacer finger springs found on the fuel prep machines, AR 935833935833
- Unit 1, power range neutron monitoring system implementation, bypass mode selector switch on October 16, 2007; and
- Common, plant risk during station blackout (SBO) maintenance.
b. Findings
No findings of significance were identified.
==1R15 Operability Evaluations (71111.15 - 4 Samples)
a. Inspection Scope
==
The inspectors reviewed operability determinations that were selected based on risk insights, to assess the adequacy of the evaluations, the use and control of compensatory measures, and compliance with the TSs. In addition, the inspectors reviewed the selected operability determinations to verify whether the determinations were performed in accordance with NDAP-QA-0703, "Operability Assessments." The inspectors used the TSs, Technical Requirements Manual, Final Safety Analysis Report (FSAR), and associated Design Basis Documents as references during these reviews.
The issues reviewed included:
- Units 1 and 2, error in critical power correlations, Part 21 - error in power prediction for partial length fuel rods, CR 900301;
- Unit 1, reactor water cleanup (RWCU) isolation on differential flow during cool down, AR 910150910150and 911162;
- Unit 1, chemistry technician de-energized the Unit 1 containment radiation monitor (CRM) instead of the Unit 2 CRM, CR 918927; and
- Unit 1 reactor fuel spacer sections found on the fuel prep machines, AR 935833935833
Revision 0.
b. Findings
No findings of significance were identified.
==1R19 Post-Maintenance Testing (71111.19 - 5 Samples)
a. Inspection Scope
==
The inspectors observed portions of post-maintenance testing activities in the field to determine whether the tests were performed in accordance with the approved procedures. The inspectors assessed the test adequacy by comparing the test methodology to the scope of maintenance work performed. In addition, the inspectors evaluated acceptance criteria to determine whether the test demonstrated that components satisfied the applicable design and licensing bases and TS requirements.
The inspectors reviewed the recorded test data to determine whether the acceptance criteria were satisfied. The post-maintenance testing activities reviewed included:
- Unit 1, core spray valve F015A dynamic motor-operated valve (MOV) testing following stem nut replacement, CR 907518;
- Unit 1, HV15768 loss-of-coolant-accident isolation testing following relay replacement, AR 906719906719
- Unit 1, HPCI quarterly flow verification after maintenance, SO-152-002;
- Unit 1, CRD stroke timing adjustments, TP-055-015; and
- Unit 2, (2D673) testing of battery charger following failure and loaded 24V battery for >6 hours.
b. Findings
No findings of significance were identified.
==1R20 Refueling and Other Outage Activities
a. Inspection Scope
==
The inspectors reviewed the outage risk management plan for the Unit 1 outage for fuel assembly rechanneling, conducted from October 12, 2007 to October 29, 2007, to confirm that PPL had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured defense-in-depth barriers. Inspectors observed the reactor shutdown including the control rods which were slow to settle and the associated control rod inoperabilities as described in Event Notification 43722 and Condition Report 918927. During the rechanneling outage, the inspector observed or reviewed the outage activities listed below.
- Establishment of a reactor vessel cool down rate;
- Establishment of shutdown cooling using the 'A' residual heat removal system;
- Outage configuration controls including:
1)availability and accuracy of reactor coolant system instrumentation;
2)availability of nuclear instrumentation;
3)electrical power alignments;
4)decay heat removal system operation;
5)availability of reactor inventory makeup water systems; and
6)secondary containment controls and integrity.
- Drywell walkdown after shutdown and prior to final closeout;
- Fuel bundle rechanneling work on the refueling floor; and
- Core verification, and reactor startup, control rod scram time tests, and reactor power increases before and after placing the turbine generator online.
In addition to the above, inspectors performed an inspection sample as recommended by Operating Experience Smart Sample (OpESS) FY2007-03, Crane and Heavy Lift Inspection, Supplemental Guidance for IP-71111.20. Inspectors verified the applicable requirements related to heavy load lifts and crane inspections. Inspectors witnessed heavy load lifts and verified the procedures enforced safety and were in agreement with PPLs prior commitments.
During the conduct of the maintenance outage activities, the inspectors reviewed the associated documentation to ensure that the tasks were performed in accordance with plant TS requirements and operating procedures. Documents reviewed are listed in the attachment to this report.
b. Findings
No findings of significance were identified.
==1R22 Surveillance Testing (71111.22 - 5 Samples)
a. Inspection Scope
==
The inspectors observed portions of selected surveillance test activities in the control room and in the field and reviewed test data results. The inspectors compared the test results to the established acceptance criteria and the applicable TS or Technical Requirements Manual operability and surveillance requirements to evaluate whether the systems were capable of performing their intended safety functions. The observed or reviewed surveillance tests included:
- Unit 1, scram time measurement of control rods, SR-155-004;
- Unit 2, compliance with SR 3.6.2.1.1 suppression pool temperature, SO-200-001;
- Unit 2, Containment Radiation Monitor monthly functional test, SC-273-102; and
- Station portable diesel generator unloaded run, OP-002-001.
b. Findings
No findings of significance were identified.
==1R23 Temporary Plant Modifications (71111.23 - 2 Samples)
a. Inspection Scope
==
The inspectors reviewed a temporary plant modification to determine whether the temporary change adversely affected system or support system availability, or adversely affected a function important to plant safety. The inspectors reviewed the associated system design bases, including the FSAR, TSs, and assessed the adequacy of the safety determination screenings and evaluations. The inspectors also assessed configuration control of the temporary changes by reviewing selected drawings and procedures to verify that appropriate revisions had been made. The inspectors compared the actual installations to the temporary modification documents to determine whether the implemented changes were consistent with the approved documents. The inspectors reviewed selected post-installation test results to determine whether the actual impact of the temporary changes had been adequately demonstrated by the test.
The following temporary modifications were reviewed:
- Station control structure chiller OK112B hi bearing temperature trip elimination; and
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation (71114.06 - 1 Sample)
a. Inspection Scope
The inspectors reviewed the combined functional drill scenario (2007 Blue Team HP Drill) that was conducted on November 13, 2007, and observed selected portions of the drill at the simulator control room and technical support center. The inspection focused on PPLs ability to properly conduct EAL classification, notification, and protective action recommendation activities and on the evaluators ability to identify observed weaknesses and/or deficiencies within these areas. Eight performance indicator (PI) opportunities were included in the scenario. The inspectors attended the evaluators post-drill critique and compared identified weaknesses and deficiencies against those identified by PPL to determine whether PPL was properly identifying failures in these areas.
b. Findings
No findings of significance were identified.
RADIATION SAFETY
Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiologically Significant Areas (71121.01 - 6 Samples)
a. Inspection Scope
The inspectors reviewed licensee activities during the Unit 1 mid-cycle fuel channel replacement outage. Particular attention was focused on the licensees use and control of contractor personnel to perform work around irradiated components in locked high and very high radiation areas. Activities observed included fuel channel removal and valve work and repair.
The inspectors reviewed the licensees self-assessments, audits, Licensee Event Reports, and Special Reports related to the access control program since the last inspection. The inspectors determined whether identified problems were entered into the corrective action program for resolution.
The inspectors reviewed radiological problem reports since the last inspection which found that the cause of the event was due to radiation worker errors. The inspectors determined if there was an observable pattern traceable to a similar cause. The inspectors determined if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. The inspector discussed with the radiation protection manager any problems with the correction actions planned or taken.
The inspectors verified adequate posting and locking of entrances to high dose rate - high radiation areas, and very high radiation areas.
The inspectors reviewed radiological problem reports since the last inspection that found the cause of the event was radiation protection technician error. The inspectors determined if there was an observable pattern traceable to a similar cause. The inspector determined if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems.
b. Findings
No findings of significance were identified.
2OS2 ALARA Planning and Controls (71121.02 - 3 Samples)
a. Inspection Scope
The inspectors reviewed the assumptions and basis for the current annual collective exposure estimate. The inspectors reviewed applicable procedures to determine the methodology for estimating work activity-specific exposures and the intended dose outcome.
The inspectors determined if there had been any declared pregnant workers during the current assessment period. The inspectors reviewed the exposure results and monitoring controls employed by the licensee with respect to requirements of
The inspectors observed and reviewed outage work activities associated with the Unit 1 fuel rechanneling, radwaste filter work, drywell activities, turbine/condenser valve work and the Control Room Emergency Outside Air Supply System (CREOAS) activities.
b. Findings
Introduction:
A self-revealing finding having very low safety significance (Green) was identified due to a deficiency in the area of maintaining occupational radiation exposures as low as is reasonably achievable (ALARA). ALARA and work planning for the CREOAS modification was less than adequate resulting in collective exposure for the work to expand from 3.37 person-rem to 11.9 person-rem.
Description:
Collective exposure during the CREOAS work during the summer of 2007 significantly exceeded its initial estimate. The performance deficiency that resulted in the exposure overrun was due to significantly increased hours beyond that planned to perform the work. The root cause of the overrun was determined to be:
- (1) a failure to include contractor work hours in the ALARA planning process; and
- (2) design errors which did not properly identify bolting locations for the duct work, requiring extensive on-site rework. Susquehannas three-year rolling average is 101 Person-rem, which is below the SDP criteria of 240 person-rem for Boiling Water Reactors (BWRs), therefore, overall ALARA performance has been effective and this finding is of very low safety significance (Green). The licensee has documented this issue in condition report 886817.
Analysis:
The occupational radiation safety significance determination defines a performance deficiency as one in which the licensee fails to meet a standard and the cause was reasonably within the licensees ability to foresee or correct. The person-hours required for this work would have been significantly lower had the installation plan for the modification correctly identified mounting locations. Further, the ALARA planning for this work should have identified the significant number of hours being worked by contractor personnel. The finding is associated with the ALARA planning attribute of the radiation safety cornerstone, and affects the objective of providing adequate protection of the worker from exposure to radiation. Susquehannas three-year-rolling-average is 101 person-rem, which is below the SDP criteria of 240 person-rem for BWRs, therefore, this finding is of very low safety significance.
Enforcement:
Traditional enforcement is not applicable since these matters did not have an actual safety consequence, or the potential for impacting the NRCs ability to perform its regulatory function. As aggregated, these matters are considered more than minor since each issue is comparable to a more than minor ALARA example described in IMC 0612, Appendix E. While no significant exposure was received by any one of the affected workers, the Significance Determination Process applies because the occurrence involved collective dose that resulted from the licensees inability to properly plan and control work during a refueling outage (ALARA planning example of the Program and Process attribute). The finding was determined to be of low safety significance (Green) because it did not involve issues involving access to radiologically significant areas; did not result in, nor was there a substantial potential for, an overexposure; and the licensees ability to assess dose was not compromised. The finding was entered into the licensees corrective action program. The finding is associated with the ALARA planning attribute of the radiation safety cornerstone, and affects the objective of providing adequate protection of the worker from exposure to radiation.
The ALARA rule contained in 10 CFR 20.1101(b) Statements of Consideration indicates that compliance with the ALARA requirement will be judged on whether the licensee has incorporated measures to track and, if necessary, to reduce exposures and not whether exposures and doses represent an absolute minimum or whether the licensee has used all possible methods to reduce exposures. The overall exposure performance of the nuclear power plant is used to determine compliance with the ALARA rule. Since Susquehanna is below the three-year-rolling-average of 240 person-rem, no violation of regulatory requirements [10CFR20.1101(b)] has occurred. (FIN 05000387/2007005-02, 05000388/2007005-02, Failure to Maintain Occupational Radiation Exposure As Low As Reasonably Achievable During CREOAS Work)
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03 - 4 Samples)
a. Inspection Scope
The inspectors verified the calibration, operability, and alarm setpoints of several types of instruments and equipment. Verification methods included review of calibration documentation, and observation of licensee source check or calibrator exposed readings. The inspectors determined what actions were taken when, during calibration or source checks, an instrument is found significantly out of calibration (>50%). The inspectors determined possible consequences of instrument use since last successful calibration or source check. The inspectors determined if out of calibration results were entered into the corrective action program.
For repetitive deficiencies or significant individual deficiencies in problem identification and resolution identified above, the inspectors determined if the licensees self-assessment activities were also identifying and addressing these deficiencies. No issues of this type were identified by the inspectors.
Based on FSAR, TSs and Emergency Operating Procedures requirements, the inspectors reviewed the status and surveillance records of self-contained breathing apparatus (SCBAs) staged and ready for use in the plant. The inspectors reviewed the licensees capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions. The inspectors determined if control room operators and other emergency response and radiation protection personnel were trained and qualified in the use of SCBA (including personal bottle change-out). The inspectors determined if personnel assigned to refill bottles were trained and qualified for that task.
The inspectors reviewed the qualification documentation for onsite personnel designated to perform maintenance on the vendor-designated vital components, and the vital component maintenance records for three SCBA units currently designated as ready for service. For the same three units, the inspectors ensured that the required, periodic air cylinder hydrostatic testing was documented and up to date, and the Department of Transportation required retest air cylinder markings were in place.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
(71151 - 19 Samples)
a. Inspection Scope
The inspectors reviewed PPLs performance indicator (PI) data, for the period of December 2006 through November 2007, to verify whether the PI data was accurate and complete. The inspectors examined selected samples of PI data, PI data summary reports, and plant records. The inspectors compared the PI data against the guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline. The following performance indicators were included in this review:
Initiating Event Performance Indicators
- Units 1 and 2 scrams with complications.
Mitigating Systems Performance Indicators (MSPI)
- Units 1 and 2 safety system functional failures;
- Units 1 and 2 MSPI index - high pressure injection systems;
- Units 1 and 2 MSPI index - heat removal systems;
- Units 1 and 2 MSPI index - residual heat removal systems; and
- Units 1 and 2 MSPI index - cooling water systems.
b. Findings
No findings of significance were identified.
Cornerstone: Physical Protection
a. Inspection Scope
The inspector performed a review of PI data submitted by the licensee for the Physical Protection Cornerstone. The review was conducted of the licensees programs for gathering, processing, evaluating, and submitting data for the Fitness-for-Duty, Personnel Screening, and Protected Area Security Equipment PIs. The inspector verified that the PIs had been properly reported as specified in Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5. The review included the licensees tracking and trending reports, personnel interviews and security event reports for the PI data collected since the last security baseline inspection. The inspector noted from the licensees submittal that there were no reported failures to properly implement the requirements of 10 CFR 73 and 10 CFR 26 during the reporting period. This inspection activity represents the completion of three
- (3) samples relative to this inspection area; completing the annual inspection requirement.
b. Findings
No findings of significance were identified.
Cornerstone: Occupational Radiation Safety (1 Sample)
a. Inspection Scope
The inspectors reviewed all licensee PIs for the Occupational Exposure Cornerstone for follow-up. The inspectors reviewed a listing of licensee action reports for the period January 1, 2007 through November 26, 2007, for issues related to the occupational radiation safety performance indicator, which measures non-conformances with high radiation areas greater than 1R/hr and unplanned personnel exposures greater than 100 mrem total effective dose equivalent (TEDE), 5 rem skin dose equivalent (SDE),1.5 rem lens dose equivalent (LDE), or 100 mrem to the unborn child.
The inspectors determined if any of these PI events involved dose rates >25 R/hr at 30 centimeters or >500 R/hr at 1 meter. If so, the inspectors determined what barriers had failed and if there were any barriers left to prevent personnel access. For unintended exposures >100 mrem TEDE (or >5 rem SDE or >1.5 rem LDE), the inspector determined if there were any overexposures or substantial potential for overexposure.
b. Findings
No findings of significance were identified.
Cornerstone: Public Radiation Safety (1 Sample)
a. Inspection Scope
The inspectors reviewed a listing of licensee action reports for the period January 1, 2007 through November 26, 2007, for issues related to the public radiation safety performance indicator, which measures radiological effluent release occurrences per site that exceed 1.5 mrem/qtr whole body or 5 mrem/qtr organ dose for liquid effluents; or 5 mrads/qtr gamma air dose, 10 mrads/qtr beta air dose; or 7.5 mrems/qtr organ doses from I-131, I-133, H-3 and particulates for gaseous effluents.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
(71152 - 1 Semi-Annual Sample and 2 Annual Samples)
.1 Review of Items Entered into the Corrective Action Program
a. Inspection Scope
As required by Inspection Procedure (IP) 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed screening of all items entered into PPLs corrective action program. This was accomplished by reviewing the description of each new action request/condition report and attending daily management meetings.
b. Findings
No findings of significance were identified.
.2 Semi-Annual Review to Identify Trends
a. Inspection Scope
As required by IP71152, Identification and Resolution of Problems, the inspectors performed a semi-annual review of PPLs corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. This trend review considered the results of daily inspector corrective action program item screenings discussed in Section 4OA2.1. The review also included issues described in system health reports, corrective maintenance work orders, PPL management meetings, regional inspector exit meetings, and maintenance rule assessments. This review concentrated on the six-month period of July 2007 through December 2007, although some examples were prior to this time period to confirm potential trends. The inspectors compared and contrasted their results with the results in PPLs internal assessment reports and trending. Corrective actions that were initiated in response to inspector observations and the issues identified in PPL trend reports were also reviewed.
b. Findings and Observations
No findings of significance were identified.
Procedure Use and Compliance
The inspectors identified an adverse trend in the area of procedure use and compliance.
Specifically, inspectors found an increase in the number of minor procedure violations and inspection items with procedure use and compliance contributors during baseline inspection activities. Procedure use issues were observed and documented in the corrective action system for multiple work groups. This identified potential trend was communicated to PPL.
PPL also identified this potential trend during internal functional group assessments, entered the issue into the corrective action program, and performed a common cause analysis for some of the more recent examples during the last quarter of 2007.
As previously documented in Inspection Report 2007-003, PPL issued an internal communication (Hot Box 07-07) on June 29, 2007, to increase worker awareness of the observed trend in human performance issues related to procedural compliance and usage. One of these examples was from inspectors witnessing non-licensed operators aligning the E EDG without utilizing one of the established step-by-step operating procedures. (NCV 2007003-01, PIM #78972)
Inspectors identified other instances of procedure use issues in the electrical maintenance, chemistry, operations and engineering departments during the second half of 2007. For example:
- In July 2007 after PPL identified reactor building scaffolding that was not built to specifications, inspectors identified additional reactor building scaffolds that were not built according to procedures and standards.
- During a December 2007 post-maintenance testing inspection, the inspectors questioned whether equipment operators were observing stabilizer valve flow indications as described by the control rod drive testing procedure. The Control Rod Drive (CRD) system engineer responded that there was an open Action Request to provide clarification to this procedure. The inspectors found that an action request was previously written to document a previous NRC inspectors question on this same issue.
- During a NRC Performance Indicator (PI) inspection, the inspectors identified that PI records were not retained or readily retrievable as required by PPL procedures. Although a performance issue, the inspectors determined that the required information was sufficient to support the inspection
PPL also identified human performance procedure related issues through the 3rd quarter 2007 Operations department functional unit excellence plan (AR 908670908670. The inspectors also determined that some of the procedure use and adherence issues observed during the 4th quarter were administrative or documentation related, and none of the individual issues were found to be of more than minor significance.
Increase in Control Room Alarm Panel Condition Reports and Emergent Work
Inspectors identified a potential adverse trend in control room alarm panel performance.
The adverse trend challenges the operations staff by making it more difficult to assess plant parameters and system performance. When alarm system power supplies failed, operators were increasing their monitoring of local field panels to compensate for the associated control room alarms for that system or train being inoperable. The number of plant annunciator system condition reports is considered to be on an increasing trend.
Inspectors categorized this observation as a potential adverse trend because there is no system health report, there were no system engineering journal entries for this system, and condition reports related to the plant annunciator systems were not typically coded to the system number which made relevant condition report retrieval and trending difficult.
This PI&R trend review documents the identified adverse trend in procedure use and adherence as well as a potential adverse trend in control room annunicator system performance at Susquehanna. These observations were not more-than-minor performance deficiencies that affected any safety cornerstone during the inspection period. Inspector observations were communicated to PPL at weekly management meetings and the quarterly exit meeting.
.3 Human Performance
- Work Control, Work Package Quality and Supervisory Oversight (1 Annual Sample)
a. Inspection Scope
The inspectors reviewed PPLs corrective actions to resolve a station-wide trend of human performance deficiencies, focused in the areas of work control, work package quality, and supervisory oversight. The inspectors reviewed several CRs, internal assessments and evaluations, conducted several interviews, observed various shift turnover meetings and pre-job briefs, and observed a sample of work activities in the field. Specifically, CR 886646 documents a common issue analysis with respect to human performance, and assigns several corrective actions as well as evaluations of the actions taken. CR 886871 documents an in-progress effectiveness review of actions taken to resolve the human performance issues. The inspectors also reviewed a recent station assessment of human performance tools, as well as actions taken to improve station use of such tools. Finally, CR 891288 documents actions taken to correct the causes of two NRC Green Findings and two NRC Green NCVs in the area of Radiation Safety, as discussed in NRC Integrated Inspection Report 05000387/2007003 and 050000388/2007003. All four Radiation Safety issues were determined to be caused by breakdowns in human performance.
The inspectors assessed PPLs problem identification threshold, cause analysis, extent of condition reviews, effectiveness reviews, internal assessments, and prioritization and timeliness of corrective actions to determine whether PPL was appropriately identifying, characterizing, and correcting problems associated with this issue. Additionally, inspectors assessed whether the planned or completed corrective actions were appropriate.
b. Findings and Observations
No findings of significance were identified.
Assessment - Control of Station Work, Work Package Quality, & Supervisory Oversight
The inspectors determined that PPL is engaging significant effort across the station with respect to control of work, work package quality, and supervisory oversight. Many corrective actions have been taken to address the deficiencies, and several corrective actions are currently ongoing. The Maintenance Department has led the corrective action effort, through the hiring of an independent contractor to perform coaching and training in human performance, focusing their effort on supervisory oversight. Inspectors observed that maintenance supervisors are being trained on the importance of implementing several standards, including in-field walkdowns and observations, procedural use and adherence, work package review, and coaching to change behavior.
The independent contractor training and coaching was also implemented within the Work Planning Department. Additional corrective actions in the area of work package quality include actions to improve procedure quality and assigning additional personnel to support procedure writing.
PPL has implemented a plan to capture the lessons learned from the contractor training and coaching efforts, and implemented these efforts across other departments at the station. CRA 919156 addresses implementation of the contractor training within the Radiation Protection Department, one of several actions to correct the NRC Green Findings and NCVs in the area of Radiation Protection (RP). Additional actions include a focus on improving occupational radiation dose estimates for work activities required to be performed, supervisory reinforcement of radiation work permit (RWP) reviews, and establishing plans to include RP supervision in outage control center (OCC) reviews.
Inspectors have observed improving trends with respect to station work package quality, and supervisory oversight. In contrast, however, inspectors have also observed a recent increase in the number of issues where there is a failure to follow procedures. This trend was confirmed after inspectors performed the semi-annual PI&R trend review in November 2007. PPL has also identified the negative trend in procedure use and adherence, and recently performed a station assessment on the use of human performance tools - including procedure use and adherence.
Since procedure use and adherence is a specific human error barrier, inspectors performed an additional PI&R annual sample on Procedure Use and Adherence during the last quarter of 2007. Inspector review of this assessment found that PPL identified similar results and trends when compared to results of previously performed assessments in the areas of work control and supervisory oversight, as mentioned above. The inspectors observed no current plan in place for PPL to integrate the results and planned corrective actions from the recent station assessment on use of human performance tools with assessments performed in the areas of work control, work package quality, and supervisory oversight.
.4 Human Performance - Procedural Use and Adherence
(1 Annual Sample)
a. Inspection Scope
The inspectors reviewed PPLs corrective actions to address issues which are related to the station-wide trend of procedure use and adherence as identified during both Semi-annual PI&R trend reviews in 2007 and also indicated during the preparation for the PI&R annual sample inspection on Work Package Quality, and Supervisory Oversight performed in December of 2007. The inspectors reviewed several CRs, internal assessments and evaluations, conducted several interviews, observed the December 2007 Management Briefing on Worker Usage of Human performance Tools (QA Assessment) and observed ongoing work activities in the field.
Inspectors identified numerous examples of procedure and work instruction non-compliance during the semi-annual PI&R trend review completed in late November 2007. In addition to the examples of procedure use and adherence issues documented under that baseline inspection effort, inspectors found additional procedure use performance issues. Inspectors used these additional examples to assess PPLs problem identification threshold, cause analysis, extent of condition reviews, effectiveness reviews, internal assessments, and prioritization and timeliness of corrective actions to determine whether PPL was appropriately identifying, characterizing, and correcting problems associated with procedure usage and adherence. Additionally, inspectors assessed whether the planned or completed corrective actions were appropriate.
b. Findings
No findings of significance were identified.
Assessment - Human Performance - Procedural Use and Adherence
One issue identified on November 26, 2007, was an open jumper test switch found in Upper Relay Room Panel 1C621 which was not removed following previous RCIC system and logic functional testing performed in October 2007. Inspectors reviewed PPLs corrective actions including cause analysis, extent of condition, and timeliness of corrective actions. Inspectors found that PPL utilized a Level 2 Cause evaluation in the corrective action system and that PPL conducted Event and Accountability Review Boards in early December. Inspectors observed a detailed review of extent of condition and apparent causes associated with the issue. This human performance issue and corrective actions will also be reviewed by the PPL Corrective Action Review Board.
Although no effectiveness review was conducted for this specific issue, PPL initiated a common cause evaluation for engineering testing errors that have occurred in 2007.
The issue is documented and tracked under CR #927706.
Inspectors also reviewed a self-revealing issue from November 12, 2007, involving a Chemistry technician securing the containment radiation monitor on the incorrect unit.
Although the human performance issues for this event and condition report are broader than procedure compliance, inspectors determined that improved use of procedures regarding filed actions and pre-job briefings and better communication practices could have prevented this event. Inspectors found that PPL performed a detailed review and evaluation of the extent of condition and apparent cause of the event. This human performance issue and corrective actions were reviewed by the PPL Corrective Action Review Board. The issue is documented and tracked under CR # 918927.
Inspectors found that PPL was using the Corrective Action Program to identify, evaluate, and correct conditions adverse to quality. Inspectors found an appropriate level of effort and priority for issues that involved procedure compliance as a contributing or apparent cause.
Although each case of a procedure non-compliance mentioned in this PI&R assessment was determined to be a performance issue, the inspectors determined that the issues were licensee-identified, had been placed in the corrective action program, and were not of more-than-minor significance. One exception, however, was a licensee-identified procedure violation that did negatively affect safety cornerstone objectives regarding unqualified seismic material left in the Unit 1 residual heat removal pump room.
Overall Assessment for PI&R Annual Samples
The inspectors determined that PPL is appropriately identifying problems in the areas of human performance - specifically, work control, work package quality, supervisory oversight, as well as, procedure use and adherence. Characterization and evaluation of the problems is generally appropriate, though inspectors observed no current plan for PPL to integrate the results and planned corrective actions from the recent station assessment on use of human performance tools with the independent assessments performed in the areas of work control, work package quality, and supervisory oversight.
Procedure use and adherence appears to be on a negative trend as compared to the other human performance barriers and tools which do not show the same adverse or negative trend. Inspectors have determined corrective actions taken to address the issues thus far have been appropriate, however, several corrective actions are currently ongoing and the inspectors will continue to monitor station performance.
4OA6 Meetings, Including Exit
On January 17, 2007, the inspectors presented their findings to Mr. C. Gannon, Vice President - Nuclear Operations, and other members of his staff, who acknowledged the findings.
4OA7 Licensee-Identified Violations
The following violation of very low safety significance (Green) was identified by PPL and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited Violation.
On October 30, 2007, PPL identified a 4-foot long I-beam in the overhead of the Unit 1 A Residual Heat Removal (RHR) pump room which was determined to be an unapproved field change, a violation of Technical Specifications 5.4.1, and a violation of those procedures that must be implemented for performing maintenance as delineated in Regulatory Guide 1.33. PPL procedure NDAP-QA-0502, Work Order Process, requires that equipment shall be returned to the original design configuration following work completion unless a change mechanism has been issued. Contrary to the above, a 4-foot I beam of approximately 80 pounds which was bridging across permanent structural steel in the Unit 1 A RHR room overhead was not removed following its use for maintenance activities. The I-beam (located 15 feet above safety related equipment)reduced the reliability of mitigating equipment regarding RHR design basis functions required following a seismic event. PPL evaluated the condition of the structural steel member and two C-clamp restraints and determined that the beam was unlikely to become dislodged during a seismic event. The beam was promptly removed and PPL entered this issue into the corrective action process (CR # 915409). The finding was determined to be very low safety significance (Green) because the probability of a dynamic event (earthquake) is very low, the as-found configuration of the structural steel member provided some resistance to falling during a dynamic event including a design basis earthquake, and although the identified deficiency reduced design margin, there was no actual loss of safety related functions.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- D. Brophy, Acting Regulatory Affairs Supervisor
- P. Capotosto, Supervising Engineer, Electrical Engineering
- D. DAngelo, Manager Station Engineering
- S. Davis, Senior Engineer, Programs and Components
- J. Helsel, Manager Nuclear Operations
- C. Hoffman, Manager, Nuclear Fuels
- J. Jeanguenat, ESW System Engineer
- W. Kahler, Senior Engineer, Nuclear Fuels
- R. Kessler, Senior Health Physicist - ALARA
- G. Machalick, Senior Engineer, Programs and Components
- F. Negvesky, Senior Engineer
- J. Pacioti, Security Operations Coordinator
- V. Schuman, Radiological Protection Manager
- M. Sleigh, Security Manager
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
None.
Opened/Closed
- 05000387, 388/2007005-01 NCV Inadequate Design Control to
Support Fuel Rechanneling Activities (Section IR12)
- 05000387, 388/2007005-02 FIN Failure to Maintain Occupational Radiation
Exposure As Low As Reasonably
Achievable During CREOAS Work (Section 2OS2)
Closed
BASELINE INSPECTION PROCEDURE PERFORMED
7112101 Access Control
2OS1 7112102 ALARA Planning and Controls
2OS2 7112103 Radiation Monitoring Instrumentation
2OS3 71151 Performance Indicator Verification
4OA1