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| number = ML11257A034
| number = ML11257A034
| issue date = 09/15/2011
| issue date = 09/15/2011
| title = 09/15/11 Proposed Meeting Slides for Forthcoming Meeting with Tennessee Valley Authority Regarding Status of Extended Power Uprate Submittal
| title = Proposed Meeting Slides for Forthcoming Meeting with Tennessee Valley Authority Regarding Status of Extended Power Uprate Submittal
| author name =  
| author name =  
| author affiliation = Tennessee Valley Authority
| author affiliation = Tennessee Valley Authority
Line 20: Line 20:


===Introductions===
===Introductions===
Background Containment Accident Pressure Replacement Steam Dryers Submittal and Review Schedule NFPA 805 Transition Status 1
===Background===
Containment Accident Pressure  
 
Replacement Steam Dryers
 
Submittal and Review Schedule
 
NFPA 805 Transition Status 1


===
===
Background===
Background===
Browns Ferry Nuclear (BFN) Extended Power Uprate (EPU) application currently under NRC review for all three units will result in 14.3 percent increase above current licensed power.
Browns Ferry Nuclear (BFN) Extended Power Uprate (EPU) application currently under NRC review for all three units will result in 14.3 percent increase above current licensed power.
In September 2009, the NRC placed the application review on hold pending development of guidance on credit for Containment Accident Pressure (CAP).
In September 2009, the NRC placed the application review on hold pending development of guidance on credit for Containment Accident Pressure (CAP).
Two outstanding issues for the BFN EPU remained to be resolved:
Two outstanding issues for the BFN EPU remained to be resolved:
    - CAP
CAP Steam dryers  
    - Steam dryers TVA met with NRC on December 15, 2010 to:
 
    - Confirm outstanding project scope
TVA met with NRC on December 15, 2010 to:
    - Communicate planned CAP mitigation strategy relative to draft NRC guidelines
Confirm outstanding project scope Communicate planned CAP mitigation strategy relative to draft NRC guidelines Communicate plans for steam dryers 2
    - Communicate plans for steam dryers 2


Background (continued)
Background (continued)
NRC guidance associated with CAP:
NRC guidance associated with CAP:
    - In January 2011, NRC Staff requested approval to resume review of EPU license amendment requests (LARs) using the revised CAP guidance.
In January 2011, NRC Staff requested approval to resume review of EPU license amendment requests (LARs) using the revised CAP guidance.
    - In March 2011, the Commissioners issued a memorandum that approved the revised CAP guidance provided by the Staff and allowed work on EPU LARs to resume.
In March 2011, the Commissioners issued a memorandum that approved the revised CAP guidance provided by the Staff and allowed work on EPU LARs to resume.
 
Based on issuance of NRC guidance on CAP, TVA determined that submittal of key assumptions (as discussed in December 15, 2010 meeting) was not necessary.
Based on issuance of NRC guidance on CAP, TVA determined that submittal of key assumptions (as discussed in December 15, 2010 meeting) was not necessary.
On May 15, 2011, the NRC issued a letter to TVA stating that, based on development of CAP review criteria, the NRC is prepared to resume review of the BFN EPU application.
On May 15, 2011, the NRC issued a letter to TVA stating that, based on development of CAP review criteria, the NRC is prepared to resume review of the BFN EPU application.
3
3


Containment Accident Pressure TVA identified and evaluated changes/modifications to eliminate or minimize CAP credit for limiting events, using NRC CAP guidance.
Containment Accident Pressure
At this time, using NPSHr (net positive suction head required) 3 percent curves eliminates CAP credit for the station blackout (SBO) and anticipated transient without scram (ATWS) events.
 
TVA identified and evaluated changes/modifications to eliminate or minimize CAP credit for limiting events, using NRC CAP guidance.
 
At this time, using NPSHr (net positive suction head required) 3 percent curves eliminates CAP credit for the station blackout (SBO) and anticipated transient without scram (ATWS) events.  
 
The following actions are planned to eliminate CAP credit for fire events:
The following actions are planned to eliminate CAP credit for fire events:
    - TVA plans to revise the Generic Letter 89-13 heat exchanger analysis and program to support taking credit for improved residual heat removal (RHR) heat exchanger performance.
TVA plans to revise the Generic Letter 89-13 heat exchanger analysis and program to support taking credit for improved residual heat removal (RHR) heat exchanger performance.
    - TVA plans to increase suppression pool inventory using Condensate Storage Tank water.
TVA plans to increase suppression pool inventory using Condensate Storage Tank water.
    - Increased suppression pool water inventory combined with improved RHR heat exchanger performance reduces peak suppression pool temperature, increases RHR pump static head, and eliminates CAP credit.
Increased suppression pool water inventory combined with improved RHR heat exchanger performance reduces peak suppression pool temperature, increases RHR pump static head, and eliminates CAP credit.
4
4


Containment Accident Pressure (continued)
Containment Accident Pressure (continued)
NRC CAP credit guidance introduced an uncertainty adder to NPSHr for a design basis loss-of-coolant accident (LOCA) event. The Boiling Water Reactor Owners Group (BWROG) has been developing a generic approach for addressing the NPSH uncertainty adder.
 
TVA plans to use the BWROG approach.
NRC CAP credit guidance introduced an uncertainty adder to NPSHr for a design basis loss-of-coolant accident (LOCA) event. The Boiling Water Reactor Owners Group (BWROG) has been developing a generic approach for addressing the NPSH uncertainty adder.  
 
TVA plans to use the BWROG approach.  
 
Improving RHR heat exchanger performance eliminates CAP credit for the long-term (i.e., >10 minutes) LOCA event.
Improving RHR heat exchanger performance eliminates CAP credit for the long-term (i.e., >10 minutes) LOCA event.
TVA plans to take CAP credit only for the short-term (i.e., <10 minutes) LOCA event in accordance with the NRC guidance.
TVA plans to take CAP credit only for the short-term (i.e., <10 minutes) LOCA event in accordance with the NRC guidance.
TVA will request formal NRC acceptance of the analysis for CAP credit for short-term LOCA.
TVA will request formal NRC acceptance of the analysis for CAP credit for short-term LOCA.
5
5
Line 59: Line 78:
Containment Accident Pressure (continued)
Containment Accident Pressure (continued)
The following summarizes the CAP credit approach for the BFN EPU application:
The following summarizes the CAP credit approach for the BFN EPU application:
Event                         Current Need                                       Approach Request formal NRC acceptance of CAP Short-term LOCA Need CAP credit for RHR and Core Spray due to run-out credit
Event Current Need Approach Short-term LOCA
(< 10 minutes)  flow rate and suction strainer loading Long-term LOCA                                                         Eliminate CAP by improving RHR heat Need small amount of CAP credit for Core Spray
(< 10 minutes)
(> 10 minutes)                                                        exchanger performance Eliminate CAP by improving RHR heat Fire Protection Need large amount of CAP credit for RHR               exchanger performance and increasing suppression pool inventory SBO       CAP credit not required                               CAP credit not required ATWS       CAP credit not required                               CAP credit not required 6
Need CAP credit for RHR and Core Spray due to run-out flow rate and suction strainer loading Request formal NRC acceptance of CAP credit Long-term LOCA
(> 10 minutes)
Need small amount of CAP credit for Core Spray Eliminate CAP by improving RHR heat exchanger performance Fire Protection Need large amount of CAP credit for RHR Eliminate CAP by improving RHR heat exchanger performance and increasing suppression pool inventory SBO CAP credit not required CAP credit not required ATWS CAP credit not required CAP credit not required 6
 
Replacement Steam Dryers
 
In December 2009, TVA determined that NRC concerns with analyses of existing steam dryers could not be resolved, and replacement steam dryers (RSDs) would be required.


Replacement Steam Dryers In December 2009, TVA determined that NRC concerns with analyses of existing steam dryers could not be resolved, and replacement steam dryers (RSDs) would be required.
An RSD specification was developed and provided to prospective vendors.
An RSD specification was developed and provided to prospective vendors.
The RSD work scope consists of three phases:
The RSD work scope consists of three phases:
    - Phase I, Design and Analysis
Phase I, Design and Analysis Phase II, Fabrication Phase III, Installation
    - Phase II, Fabrication
 
    - Phase III, Installation Negotiations are in progress with General Electric Hitachi for RSD design, analysis, fabrication, and installation.
Negotiations are in progress with General Electric Hitachi for RSD design, analysis, fabrication, and installation.
7
7


Submittal and Review Schedule The proposed EPU schedule is based on overall resource and risk considerations for TVA.
Submittal and Review Schedule
 
The proposed EPU schedule is based on overall resource and risk considerations for TVA.
 
The EPU schedule assumes the following:
The EPU schedule assumes the following:
    -  RSD analysis and design will not begin until the formal acceptance of the CAP analysis by the NRC.
RSD analysis and design will not begin until the formal acceptance of the CAP analysis by the NRC.
    -  RSD fabrication will not begin until NRC issues the EPU amendment.
RSD fabrication will not begin until NRC issues the EPU amendment.
8
8


Submittal and Review Schedule (continued)
Submittal and Review Schedule (continued)
TVA Submittals EPU CAP Analysis Report                       May 2012
TVA Submittals
    - Schedule assumes BWROG input is received in March 2012
 
    - TVA will request NRC formal acceptance of CAP Analysis Report EPU Steam Dryer Analysis Report               Spring 2014 NRC Review Expectations Acceptance of CAP Analysis Report             Spring 2013 Issue EPU Amendment                           2015 9
EPU CAP Analysis Report May 2012 Schedule assumes BWROG input is received in March 2012 TVA will request NRC formal acceptance of CAP Analysis Report
 
EPU Steam Dryer Analysis Report Spring 2014 NRC Review Expectations
 
Acceptance of CAP Analysis Report Spring 2013
 
Issue EPU Amendment 2015 9
 
NFPA 805 Transition Status Major Milestones Achieved
 
NFPA Code compliance evaluations
 
Nuclear safety capability assessment (NSCA) component selection, logics, cable selection, and cable routing (final owner reviews pending)


NFPA 805 Transition Status Major Milestones Achieved NFPA Code compliance evaluations Nuclear safety capability assessment (NSCA) component selection, logics, cable selection, and cable routing (final owner reviews pending)
Scoping fire modeling (generic treatments calculation)
Scoping fire modeling (generic treatments calculation)
Remaining Major Milestones Fire PRA completion (including peer review)
Remaining Major Milestones
Fire area assessments and variance from deterministic requirements (VFDR) resolutions Fire risk evaluations LAR preparation and submittal 10}}
 
Fire PRA completion (including peer review)
 
Fire area assessments and variance from deterministic requirements (VFDR) resolutions
 
Fire risk evaluations
 
LAR preparation and submittal 10}}

Latest revision as of 02:05, 13 January 2025

Proposed Meeting Slides for Forthcoming Meeting with Tennessee Valley Authority Regarding Status of Extended Power Uprate Submittal
ML11257A034
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 09/15/2011
From:
Tennessee Valley Authority
To: Gratton C
Office of Nuclear Reactor Regulation
Gratton, Christopher
References
Download: ML11257A034 (15)


Text

TENNESSEE VALLEY AUTHORITY BROWNS FERRY NUCLEAR PLANT Meeting with NRC Extended Power Uprate and Transition to NFPA 805 Update Rockville, Maryland September 15, 2011

Agenda

Introductions

Background

Containment Accident Pressure

Replacement Steam Dryers

Submittal and Review Schedule

NFPA 805 Transition Status 1

=

Background===

Browns Ferry Nuclear (BFN) Extended Power Uprate (EPU) application currently under NRC review for all three units will result in 14.3 percent increase above current licensed power.

In September 2009, the NRC placed the application review on hold pending development of guidance on credit for Containment Accident Pressure (CAP).

Two outstanding issues for the BFN EPU remained to be resolved:

CAP Steam dryers

TVA met with NRC on December 15, 2010 to:

Confirm outstanding project scope Communicate planned CAP mitigation strategy relative to draft NRC guidelines Communicate plans for steam dryers 2

Background (continued)

NRC guidance associated with CAP:

In January 2011, NRC Staff requested approval to resume review of EPU license amendment requests (LARs) using the revised CAP guidance.

In March 2011, the Commissioners issued a memorandum that approved the revised CAP guidance provided by the Staff and allowed work on EPU LARs to resume.

Based on issuance of NRC guidance on CAP, TVA determined that submittal of key assumptions (as discussed in December 15, 2010 meeting) was not necessary.

On May 15, 2011, the NRC issued a letter to TVA stating that, based on development of CAP review criteria, the NRC is prepared to resume review of the BFN EPU application.

3

Containment Accident Pressure

TVA identified and evaluated changes/modifications to eliminate or minimize CAP credit for limiting events, using NRC CAP guidance.

At this time, using NPSHr (net positive suction head required) 3 percent curves eliminates CAP credit for the station blackout (SBO) and anticipated transient without scram (ATWS) events.

The following actions are planned to eliminate CAP credit for fire events:

TVA plans to revise the Generic Letter 89-13 heat exchanger analysis and program to support taking credit for improved residual heat removal (RHR) heat exchanger performance.

TVA plans to increase suppression pool inventory using Condensate Storage Tank water.

Increased suppression pool water inventory combined with improved RHR heat exchanger performance reduces peak suppression pool temperature, increases RHR pump static head, and eliminates CAP credit.

4

Containment Accident Pressure (continued)

NRC CAP credit guidance introduced an uncertainty adder to NPSHr for a design basis loss-of-coolant accident (LOCA) event. The Boiling Water Reactor Owners Group (BWROG) has been developing a generic approach for addressing the NPSH uncertainty adder.

TVA plans to use the BWROG approach.

Improving RHR heat exchanger performance eliminates CAP credit for the long-term (i.e., >10 minutes) LOCA event.

TVA plans to take CAP credit only for the short-term (i.e., <10 minutes) LOCA event in accordance with the NRC guidance.

TVA will request formal NRC acceptance of the analysis for CAP credit for short-term LOCA.

5

Containment Accident Pressure (continued)

The following summarizes the CAP credit approach for the BFN EPU application:

Event Current Need Approach Short-term LOCA

(< 10 minutes)

Need CAP credit for RHR and Core Spray due to run-out flow rate and suction strainer loading Request formal NRC acceptance of CAP credit Long-term LOCA

(> 10 minutes)

Need small amount of CAP credit for Core Spray Eliminate CAP by improving RHR heat exchanger performance Fire Protection Need large amount of CAP credit for RHR Eliminate CAP by improving RHR heat exchanger performance and increasing suppression pool inventory SBO CAP credit not required CAP credit not required ATWS CAP credit not required CAP credit not required 6

Replacement Steam Dryers

In December 2009, TVA determined that NRC concerns with analyses of existing steam dryers could not be resolved, and replacement steam dryers (RSDs) would be required.

An RSD specification was developed and provided to prospective vendors.

The RSD work scope consists of three phases:

Phase I, Design and Analysis Phase II, Fabrication Phase III, Installation

Negotiations are in progress with General Electric Hitachi for RSD design, analysis, fabrication, and installation.

7

Submittal and Review Schedule

The proposed EPU schedule is based on overall resource and risk considerations for TVA.

The EPU schedule assumes the following:

RSD analysis and design will not begin until the formal acceptance of the CAP analysis by the NRC.

RSD fabrication will not begin until NRC issues the EPU amendment.

8

Submittal and Review Schedule (continued)

TVA Submittals

EPU CAP Analysis Report May 2012 Schedule assumes BWROG input is received in March 2012 TVA will request NRC formal acceptance of CAP Analysis Report

EPU Steam Dryer Analysis Report Spring 2014 NRC Review Expectations

Acceptance of CAP Analysis Report Spring 2013

Issue EPU Amendment 2015 9

NFPA 805 Transition Status Major Milestones Achieved

NFPA Code compliance evaluations

Nuclear safety capability assessment (NSCA) component selection, logics, cable selection, and cable routing (final owner reviews pending)

Scoping fire modeling (generic treatments calculation)

Remaining Major Milestones

Fire PRA completion (including peer review)

Fire area assessments and variance from deterministic requirements (VFDR) resolutions

Fire risk evaluations

LAR preparation and submittal 10