ML20140C556

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Responds to NRC Re Violations Noted in IE Insp Rept 50-413/84-36.Corrective Actions:Hydrogen Cylinders Relocated to Shed in Plant Yard & Excess Flow Valve Provided in Discharge Piping at Hydrogen Shed
ML20140C556
Person / Time
Site: Catawba Duke Energy icon.png
Issue date: 05/31/1984
From: Tucker H
DUKE POWER CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20140C515 List:
References
NUDOCS 8406190380
Download: ML20140C556 (2)


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DUKE POWER GOMPANY P.O. DOx G3180 CHAMLOTTE. N.C. 28242 HALB. TUCKER TELEPflOME May 31, 1984' Mr. James P. O'Reilly, Regional Administrator U. S. Nuclear Regulatory Commission-Region II

-101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30303-Re: RII:WHM/GRW 50-413/84-36

Dear Mr. O'Reilly:

Please find attached a response to Deviation No. 413/84-36-04, as identified in the above referenced inspection report.

Duke Power Company does not consider any information contained in this inspection report to be proprietary.

Very.truly yours, t

Yb f,g/

Hal B. Tucker LTP/php.

Attachment i

cc: NRC Resident Inspector Catawba Nuclear Station Mr. Robert Guild, Esq.

Attorney-at-Law l

P. O.-Box 12097 Charleston, South Carolina 29412 Palmetto Alliance 21353 Devine Street Columbia, South Carolina 29205 Mr. Jesse L. Riley Carolina Environmental Study Group 854 Henley Place Charlotte, North Carolina 28207 i

j 8406190380 840611

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PDR ADOCK 05000413 G

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E Response to Deviation 413/84-36-04 Corrective Actions In Duke's letter of. April '14, 1983 to. the NRC/NRR, it' was stated that in. each Reactor Building there are two (2) 150 lb. hydrogen cylinders

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and associated piping which provides a gas blanket for Reactor Coolant Pump drain tanks.

.The subject cylinders have been relocated to the hydrogen. shed in the plant yard (Ref: letter of clarification dated April-25, 1984.).

An' excess flow valve will be provided in the discharge piping at the' hydrogen shed.

flechanical systems will review pipe routing to assure that if non-seismic pipe were to fail, concentration of hydro-gen in the area would be below 2%.

This complies with the Standard Review Plan.

Also, a pressure test of this QA Condition 3 piping does

. not require QA inspection.

Status Full compliance to be achieved prior to Fuel Load.

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