ML17263A574

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Insp Rept 50-244/94-05 on 940208-0308.Violations Noted.Major Areas Inspected:Plant Operations,Maintenance,Engineering, Plant Support & Safety Assessment/Quality Verification
ML17263A574
Person / Time
Site: Ginna Constellation icon.png
Issue date: 04/05/1994
From: Lazarus W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17263A572 List:
References
50-244-94-05, 50-244-94-5, NUDOCS 9404120032
Download: ML17263A574 (68)


See also: IR 05000244/1994005

Text

U. S. NUCLEARREGULATORY COMIVHSSION

REGION I

Inspection Report 50-244/94-05

License: DPR-18

Facility:

R. E. Ginna Nuclear Power Plant

Rochester

Gas and Electric Corporation (RG&E)

Inspection:

Inspectors:

February 8 through March 8, 1994

T. A. Moslak, Senior Resident Inspector, Ginna

E. C. Knutson, Resident Inspector, Ginna

Approved by:

s,

ief, Reactor Projects Section 3B

INSPECTION SCOPE

Date

Plant operations,

maintenance,

engineering,

and plant support.

9404120032

940406

PDR

ADOCK 05000244

8

PDR

INSPECTION EXECUTIVE SU584ARY

Operations

The plant operated at 98 percent power for the majority of the inspection period.

On February

17, 1994, loss of offsite power circuit 751 caused a spurious turbine runback.

By coincidence,

the "A" EDG was operating in parallel with circuit 751 at the time.

Although this prevented

the associated

480-volt safeguard

buses from being deenergized,

the resultant undervoltage

transient caused a momentary turbine runback.

Reactor power was subsequently reduced to less

than 90 percent,

as required by technical specifications, while core axial flux distribution was

stabilized. Full power operation was resumed later that day. Operator response to the transient

was prompt and in accordance with procedure.

Actions were well-focused on establishing and

maintaining plant stability.

On March 4, 1994, the plant was shut down to commence the scheduled annual refueling outage.

At the close of the inspection period, the reactor was in refueling shutdown mode, with reactor

disassembly in progress in preparation for full core offload to support extensive service water,

component cooling water, and residual heat removal system maintenance.

Maintenance

Corrective maintenance on spent fuel pool service water system components

was well planned

to optimize plant safety for a complete core off-load. Diagnostic testing on the Turbine Driven

Auxiliary Feedwater

Pump was effectively carried out to identify and evaluate off-normal

operating parameters.

Engineering

On February

15,

1994, the licensee

determined

that the two manual containment isolation

pushbuttons had not been periodically tested as required by technical specifications.

The licensee

requested,

and was granted, enforcement discretion to defer testing until after shutdown for the

refueling outage.

In January,

1994, the licensee determined

that two containment pressure

instruments had been inoperable since June 1992 due to blockage of the common sensing line

that connects the associated

pressure transmitters with containment;

as a result, the reliability

of automatic

initiation of certain

safety

features

was

degraded.

These

two conditions

demonstrated

that testing was not being appropriately performed, and constituted a violation of

10 CFR 50, Appendix B, Criterion XI, "Test Control."

Executive Summary

Plant Support

On March 1, 1994, while purging the pressurizer to the volume control tank, valve seat leakage

in the post accident sampling system resulted in minor radioactive contamination of water in the

condensate

storage tanks; the health physics technician who discovered

the problem was also

slightly contaminated.

Licensee

response

to this minor radiological event was prompt and

comprehensive.

At the close of the inspection period, a root cause analysis of this event was

in progress.

Safety Assessment/Quality Verification

In a meeting ofthe Nuclear Safety Auditand Review Committee, topics were candidly discussed

and were presented with sufficient detail for board members to assess

the safety significance of

the agenda issues.

TABLEOF CONTF22lTS

EXECVI'IVESUMMARY

TABLE OF CONTENTS

1v

1.0

OPERATIONS (71707)

1.1

Operational Experiences

1.2

Control ofOperations....................

1.3

Spurious

Actuation of Automatic Reactor

Protection

Offsite Electrical Transient

1.4

Plant Shutdown For Cycle 24 Refueling Outage

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System

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Due To

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2.0

MAINTENANCE(62703, 61726).....

2.1

Preventive/Corrective Maintenance

2.1.1

Routine Observations....

2.2

Surveillance Observations

2.2.1

Routine Observations....

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5

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3.0

ENGINEERING (71707)

3.1

Failure to Test Containment Isolation Manual Push Buttons......

3.2

Containment

Pressure

Transmitters

Inoperable

Due to Blockage

Pressure

Sensing Line

of

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4.0

PLANT SUPPORT (71707)

4.1

Radiological Controls..........

4.1.1

Routine Observations......

4.1.2

Post Accident Sampling System

4.1.3

ALARAPlanning For Outage

4.2

Securjty

4.2.1

Routine Observations......

4.3

Fire Protection ..............

4.3.1

Routine Observations......

Material Condition

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5.0

SAFETY ASSESSMENT/QUALITY VERIFICATION....

5.1

Periodic Reports .......................

5.2

Licensee Event Reports...................

5.3

Nuclear Safety Audit and Review Committee Meeting

5.4

Regional Staff/RG&E Management Meeting ......

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6.0

ADMINISTRATIVE(71707, 30702, 94600)

6.1

Deep Backshift Inspection

6.2

ExitMeebngs.........................

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DETAILS

1.0

OPERATIONS (71707)

1.1

Operational Experiences

At the beginning of the inspection period, the plant was operating at full power (98 percent).

On February

17, 1994, a voltage transient on one of the two offsite electrical power supply

circuits resulted in a fivepercent power reduction due to momentary, transient-induced actuation

of the turbine runback functions.

Operators

subsequently

reduced power to 89 percent,

as

required by technical specifications, while core axial fluxdistribution was stabilized. Full power

operation was resumed later that day and continued until March 4, 1994, when a controlled

shutdown was performed to commence the scheduled annual refueling outage.

At the close of

the inspection period, the reactor was in refueling shutdown mode, with reactor disassembly in

progress in preparation for full core offload to support extensive service water, compone'nt

cooling water, and residual heat removal system maintenance.

1.2

Control of Operations

Overall, the inspectors

found the R. E. Ginna Nuclear Power plant to be operated

safely.

Control room staffing was as required.

Operators exercised control over access to the control

room.

Shift supervisors

maintained authority over activities and provided detailed turnover

briefings to relief crews.

Operators adhered to approved procedures

and were knowledgeable

of off-normal plant conditions.

The inspectors reviewed control room log books for activities

and trends,

observed

recorder

traces for abnormalities,

assessed

compliance with technical

specifications,

and verified equipment availability was consistent with the requirements

for

existing plant conditions.

During normal work hours and on backshifts, accessible

areas of the

plant were toured.

No operational inadequacies or concerns were identified.

1.3

Spurious

Actuation of Automatic Reactor

Protection

System

Due To Offsite

Electrical Transient

Offsite electrical power for the Ginna plant is provided by two independent 34.5 kilovoltsupply

lines, designated

circuits 751 and 767.

Each circuit supplies one of the two station auxiliary

transformers,

12A and 12B. Along with normal site loads,, these transformers each supply two

safety grade (1E) 480 volt electrical buses.

Two emergency diesel generators

(EDGs) serve as

backup 1E power sources for the auxiliary transformers.

The 1E electrical buses are safety

significant in that they supply power to reactor

safety/accident

mitigation equipment

and

instrumentation.

On February 17, 1994, operators were conducting a monthly performance test of the "A"EDG,

with the diesel loaded to 2000 KW. Since normally operating plant equipment does not provide

this much load, the EDG was being operated in parallel with circuit 751,

This electrical

alignment is specified by the performance test and allows operators

to establish the required

EDG loading by backfeeding power through circuit 751.

Concurrent with the EDG testing, a mechanical problem had developed with one of the power

distribution breakers at the offsite supply station (station 204) that supplies power forcircuit 751.

At about 2:20 PM, offsite power control initiated switching operations to isolate the affected

circuit breaker.

During this operation, malfunction of a bank of automatic close-in capacitors

produced a loss of the circuit 751 supply bus.

Since the "A"EDG was coincidentally operating

in parallel with circuit 751, it assumed all of the electrical load upon loss of the normal power

supply. This large increase in load caused the EDG voltage to drop below the undervoltage trip

setpoint of the two 1E bus normal supply breakers.

These breakers opened, thus isolating the

1E buses

(buses

14 and 18) from circuit 751, with power continuing to be supplied to these

buses by the "A" EDG.

Bus 14 supplies normal power to two of the four instrument buses which power one channel of

the reactor

protection

system.

One of these

two instrument

buses

(bus "A") receives

auctioneered power from the 125-volt DC 1E electrical distribution system, such that degradation

or loss of a single power supply will not affect power at the instrument bus.

The other

instrument bus (bus "B") is powered only by bus 14.

Therefore, while the "A" EDG was

carrying circuit 751, the degraded voltage was translated to instrument bus "B". Voltage was

sufficiently low to trip reactor protection system channel "B"protective function bistables.

Since

the reactor protection

system

turbine runback

functions

(overpower

and overtemperature

temperature difference) require only one signal to satisfy the system logic, a turbine runback

occurred during the approximately four seconds of degraded voltage operation.

The automatic turbine runback decreased

plant power to approximately 93 percent.

Although

this was a relatively small power reduction, a xenon buildup complicated the operators'fforts

to maintain allowable core flux distribution. Operators were not successful at maintaining axial

flux difference within the target band, and consequently initiated a further reduction in power

to less than 90 percent,

as required by technical specification 3.10.2.9.

The power reduction

was halted at 89 percent and axial flux difference was stabilized within the target band.

Stable offsite power was restored to circuit 751 within two minutes of the transient.

After

discussion with the load dispatcher,

operators transferred the affected 1E electrical buses back

to circuit 751 and shut down the "A"EDG. Reactor power was slowly escalated,

due to end-of-

cycle core physics constraints, with fullpower operation being achieved at 10:10 PM, February

17, 1994.

The inspector arrived at the control room several minutes after the transient started and observed

good operator

response

to the transient.

Actions per abnormal procedure

(AP)-TURB.2,

"Turbine Load Rejection," were promptly carried out. The Head Control Operator effectively

maintained focus on verifying that the necessary

equipment was operating and that conditions

were stable.

Reactor power was promptly reduced when axial flux difference exceeded

the

target band.

NRC notification was completed as required by 10 CFR 50.72.

Although good procedural

adherence

was observed,

the inspector

questioned

whether the

directions in PT-12.1, "Emergency Diesel Generator 1A," for operation of the EDG voltage

regulator and speed governor, were adequate.

During this test, EDG voltage and speed control

are selected for manual control to facilitate operation of the generator in parallel with the grid.

The procedure contains a precaution to return these controls to automatic ifa safety injection

signal were to occur during conduct of the test.

The basis of this precaution is that the normal

(offsite power) feed breakers

would open in response

to a safety injection signal, and the

generator would become the sole source of power to the associated

safeguard buses.

Although

loss of circuit 751 had produced the same result, operators left the EDG voltage and speed

control in manual,

because

the precaution

was specific to safety injection.

The inspector

discussed this question with the licensee.

The licensee agreed that the precaution for returning

the EDG voltage and speed control to automatic should be extended to a loss of offsite power.

The inspector had no additional concerns on this matter.

1.4

Plant Shutdown For Cycle 24 Refueling Outage

The inspector observed portions of the power reduction and plant shutdown that were conducted

on March 4, 1994 for the Cycle 24 refueling outage.

The inspector observed that the power

reduction was well controlled. Strict procedural adherence and good communications, including

repeat-backs of directed procedural steps, were observed.

Low power operations,

pre-outage

turbine testing, and reactor shutdown were well coordinated.

Management

involvement in

operations was evident during preparations for, and conduct of, turbine testing.

The reactor

shutdown and transition to plant cooldown were conducted deliberately and without incident.

The inspector had no additional concerns in this area.

2.0

MAINTENANCE(62703, 61726)

2.1

Preventive/Corrective Maintenance

2.1.1

Routine Observations

The inspector observed portions of maintenance activities to verify that correct parts and tools

were utilized, applicable industry code and technical specification requirements were satisfied,

adequate

measures

were in place to ensure

personnel

safety and prevent damage

to plant

structures, systems, and components, and to ensure that equipment operability was verified upon

completion.

The following maintenance activities were observed:

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Work Order (WO) 19320990, "Disassemble/Inspect/Replace

V-4622 (Spent fuelpit (SFP)

heat exchanger "A" service water outlet isolation valve), observed February 22, 1994

This is a Crane model 143'lobe valve; as discussed in inspection report 50-

244/93-12, the licensee determined that these valves are susceptible to stem/disc

separation due to failure of the stem/disc lock weld. This maintenance revealed

that the lock weld on this valve had failed, but that there was still full stem/disc

V'

engagement.

Additionally, the seat ring guide (fits around the lower valve stem

to help keep the disc centered) was found to be worn. A non-conformance report

(NCR 94-009) was issued by the Quality Assurance department to document the

deficiencies identified during this maintenance and to authorize interim use until

November 30, 1994.

The inspector considered that conducting this maintenance prior to the refueling

outage was prudent, for the following reasons:

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Maintenance was coordinated withother service water system maintenance

which required both trains of SFP cooling to be secured

to provide

isolation;

SFP cooling was secured for maintenance when the heat load was low as

possible (approximately 10 months after the last refueling outage and just

prior to the current refueling outage);

With a full core off-load to be performed during the current refueling

outage,

maintenance

performed prior to the outage improved

system

reliability.

The inspector considered that deferral ofvalve replacement

as specified by NCR

94-009 would be of minimal safety significance.

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WO 19400816,

"Turbine Driven Auxiliary Feedwater Pump - Repair Outboard Pump

Bearing," observed February 25, 1994

During routine monthly performance testing on February 24, 1994, technicians

noted that the turbine driven auxiliary feedwater

(TDAFW) pump outboard

bearing cartridge temperature increase was greater than expected.

The pump was

declared

inoperable,

pending further investigation.

The following day, after

changing

the bearing oil and inspecting the bearing cartridge,

the pump was

operated for several hours while bearing oil and cartridge temperatures

were

monitored.

Although bearing

cartridge

temperature

was still higher

than

expected,

the long monitored

run time demonstrated

that oil temperature

eventually

stabilized

within the

band

specified

in

the

vendor's

manual.

Additionally, pump vibration was monitored periodically until oil temperature

stabilized, and indicated normal operation.

Based on these results, the TDAFW

pump was declared operable on February 25, 1994.

The inspector considered that this maintenance activity was well executed.

The

inspector considered

that the licensee's

action to declare

the TDAFW pump

operable was adequately supported by the test results.

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WO 19400660,

"Perform DP Testing on MOV-4663 (Air conditioning service water

isolation)," performed per M-64.1.2, "MOVATSTesting of Motor Operated Valves,"

revision 20, effective date February 15, 1994, observed March 1, 1994

The technicians were knowledgeable oftest methods and procedural requirements.

No deficiencies were noted.

2.2

Surveillance Observations

2.2.1

Routine Observations

Inspectors observed portions of surveillances to verifyproper calibration oftest instrumentation,

use of approved

procedures,

performance of work by qualified personnel,

conformance

to

limitingconditions for operation (LCOs), and correct system restoration following testing.

The

following surveillances were observed:

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Performance

Test (PT)-2.1M, "Safety Injection System Monthly Test," revision 10,

effective date December 30, 1993, observed February 17, 1994

PT-12.1, "Emergency Diesel Generator 1A," revision 72, effective date October 26,

1993, observed February 17, 1994

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PT-50.3, "Differential Pressure

Testing of Containment Spray Valves MOV-860C and

MOV-860D," revision 1, effective date April 28, 1990, observed February 23, 1994

T-18C, "Turbine Overspeed

Trip Test," revision

16, effective date June 4,

1993,

observed March 4, 1994

The inspector determined

through observing this testing that operations

and test personnel

adhered to procedures,

test results and equipment operating parameters

met acceptance criteria,

and redundant equipment was available for emergency operation.

3.0

ENGINEERING (71707)

3.1

Failure to Test Containment Isolation Manual Push Buttons

By letter dated February 15, 1994, RG&E requested

that the NRC staff exercise discretion to

not enforce compliance with the required actions of Technical Specification (TS) Table 4.1.2,

Item No. 9, for testing the manual containment isolation push buttons, because testing at power

could potentially challenge plant engineered

safety features.

RG&E had informed the NRC by

telephone on February 14, 1994, that it had determined that the two control room push buttons,

which can be used by operators to manually actuate the containment isolation system, had not

been

tested

as part of the routine surveillance testing of that system.

On the basis of the

submitted documents,

the NRC staff concluded that postponement of performing this test until

fl

P

6

after the plant is in cold shutdown, beginning March 7, 1994, involves minor safety impact.

Therefore, discretion was exercised to delay testing until the refueling outage and not to enforce

immediate compliance with the requirement ofTS Table 4.1.2, Item No. 9, from 10:00 AMon

February

16,

1994 (the time that the limiting condition for operation for this requirement

expired) to 12:00 AMon March 7, 1994, when the plant would be in cold shutdown and the TS

requirement

would be no longer applicable.

Testing of the manual containment isolation

function willbe performed prior to resuming power operations.

The NRC staff has reviewed relevant plant procedures and supporting documentation, including

Licensee Event Report 94-04, addressing

the functional testing of both containment isolation

push buttons.

Dedicated surveillance testing of this manual function had not been performed as

required by Technical Specifications and as such, represented

failure to implement a testing

program as required by 10 CFR 50, Appendix B, Criterion XI, "Test Control."

Criterion XI

states, "Atest program shall be established to assure that all testing required to demonstrate that

structures,

systems,

and components will perform satisfactorily in service is identified and

performed in accordance with written test procedures which incorporate the requirements

and

acceptance

limits contained in applicable design documents."

Contrary to this requirement,

dedicated

testing of the manual

containment

isolation function was not incorporated

into

procedures

and implemented.

(50-244/94-05-01)

3.2

Containment Pressure Transmitters Inoperable Due to Blockage ofPressure Sensing

Line

As documented in Inspection Report 50-244/94-01, in January

1994, a control room operator

observed that one of the narrow range (0-60psig) containment pressure instruments, PI-947, was

reading slightly lower than the other two, PI-945 and PI-949.

Troubleshooting revealed the cause to be a blockage in the sensing line between containment and

the pressure

transmitter,

PT-947.

The portion of the sensing line within the containment

penetration was found to be made of carbon steel; this was the location of the blockage, which

was later determined to be rust.

Because this sensing line is shared with containment pressure

transmitter PT-948, two channels ofcontainment pressure instrumentation had been inoperable.

Review of computer-archived

data revealed that this condition had existed since June 1992.

The apparent cause ofthe blockage was that water had historically been used as the process fluid

during annual instrument calibrations.

This testing was performed by isolating the detector and

then attaching the pressure

source to a test connection within the detector isolation boundary.

Upon restoration from testing, residual water would drain from the detector, through the sensing

line, and into containment.

Exposure of the horizontal run of carbon steel tubing within the

containment penetration to this runoffwater caused rust, which, after years of service, plugged

the line. Existence of the blockage went undetected for a long period (1) because the scales of

the associated

meters were too large to show significant deflection as a result of normal

containment pressure variations, and (2) because verifying communication through the sensing

line, from the transmitters root valves to its end point inside containment, was not included in

performance testing.

The result of this problem was that it degraded the reliability of automatic initiation of certain

safety features, with the two-out-of-three (2/3) logic being reduced to two-out-of-two (2/2).

Specifically, the 2/3 logic required for a safety injection signal based on a 4 psig containment

pressure would have been reduced to a 2/2 logic with the inoperability ofP-947. However, the

diverse actuation circuitry for the safety injection signal has three additional means of actuation

(steam generator low steam pressure,

pressurizer low pressure,

and manual).

None of these

diverse means was affected by the inoperability of P-947.

The 2/3 logic required for steam line isolation actuation based on a 18 psig containment pressure

was reduced to a 2/2 logic with the inoperability of P-948.

The diverse actuation circuitry for

steam line isolation has three additional means of actuation (high steam flow, high-high steam

flowwith safety injection, and 2/4 low T-average with safety injection, and manual).

None of

these diverse features were affected by the inoperability of P-948.

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The 2/3 plus 2/3 logic required for containment spray actuation based on a 28 psig containment

pressure was reduced to a 2/2 plus 2/2 logic with the inoperability ofP-947 and P-948, however,

manual actuation was available ifrequired.

Subsequent

to identifying the plugging, the affected channels were tripped until the line was

cleared and licensee management

tasked the operations and engineering staffs to evaluate the

safety implications and implement corrective actions to preclude a recurrence.

Results of these

efforts are documented in LER 94-02, submitted to the NRC on March 4, 1994.

In reviewing LER 94-02, the inspector identified two shortcomings in the licensee

s scope of

corrective action and safety evaluation.

First, the licensee

failed to address

test program

inadequacies

that resulted in a failure to promptly identify line blockage and inoperable pressure

sensing channels.

This incident is similar in nature to that described in section 3.1 above, in

which containment isolation pushbuttons were not tested, and represented

a second example of

a violation of the requirements of 10 CFR 50, Appendix B, Criterion XI, "Test Control" (see

Detail 3.1).

The second shortcoming was that an evaluation of the effect of the loss of one (circuit 751) of

two offsite power sources

on the remaining operable pressure

channels

was not addressed.

Automatic containment spray initiation could be compromised by a loss ofcircuit 751 in certain

situations

because

such

a loss could temporarily deenergize

safety bus

14 and associated

instrument bus "B", which has no backup power supply. Instrument bus "B" powers one set of

pressure

sensing channels (PI-946 and PI-949).

Therefore, loss of instrument bus "B" could

cause

the loss of an additional two channels of containment pressure

instrumentation.

The

licensee acknowledged this design vulnerability and willaddress this evaluation in a supplement

to LER 94-02.

8

The inspector reviewed the licensee's

immediate corrective actions taken in response

to this

incident including: placing the affected pressure channel relays in the tripped position, clearing

the sensing line, daily trending narrow range containment pressure

indications on the plant

computer, revising the instrument calibration procedure

to use air rather than water as the

process fluid, and scheduling inspection of the remaining containment pressure

sensing lines

during the refueling outage.

The inspectors had no further questions at this time.

4.0

PLANT SUPPORT (71707)

4.1

Radiological Controls

4.1.1

Routine Observations

The inspectors periodically confirmed that radiation work permits were effectively implemented,

dosimetry was correctly worn in controlled

areas

and dosimeter

readings

were accurately

recorded, access to high radiation areas was adequately controlled, survey information was kept

current, and postings and labeling were in compliance Lith regulatory requirements.

Through

observations ofongoing activities and discussions with plant personnel, the inspectors concluded

, that the licensee's radiological controls were generally effective.

4.1.2

Post Accident Sampling System Material Condition

On March 1, 1994, operators established

a purge of the pressurizer

steam space to the volume

control tank, through the post-accident sample system (PASS).

The purpose of this purge was

to reduce the hydrogen concentration in the pressurizer in preparation for the refueling outage.

While this purge was in progress,

a health physics (HP) technician prepared to perform a water

flush of the PASS deionized water header.

The PASS is configured

such that these two

operations can be performed simultaneously; however, as preparatio'ns for the flush progressed,

the HP technician observed

steam coming from a flexible hose in the DI water header.

A

portable radiation survey instrument in the area of the steam discharge alarmed, indicating that

the pressurizer was the likely source of the steam.

The HP technician isolated the flexible hose

and then informed the control room operators of the problem.

Venting of the pressurizer

through the PASS was secured.

Extensive radiation and contamination surveys were performed.

The HP technician was found

to be contaminated with short-lived radioactive gases, and was decontaminated.

Radiation levels

in the vicinityof the steam leak were normal.

Some loose surface contamination was detected

on the floor in the area of the leak; the area was roped off, and subsequently

cleaned

and

decontaminated.

Since the deionized water header cross-connects

to several other radiologically

clean water systems, all connecting water systems were sampled for radioactive contamination.

Small concentrations ofradioactive gases and particulates were found in the condensate

storage

tanks.

The concentrations

were so low as to not pose a radiological concern for normal use.

No significant contamination was detected in the remaining deionized water systems associated

with this event.

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In response to this event, the licensee initiated a root cause analysis investigation.

The affected

portions of the PASS were removed from service, pending results of this investigation and

determination of corrective action. Multiplevalve seat leakage through the ih-inch line was an

apparent contributor to this event.

The inspector examined the material condition of the PASS.

The inspector noted that the existing installation ofthe air operator forvalve AOV-10017 (PASS

sample cooler outlet AOV to PASS liquid and gas sample panel), a valve that is normally shut,

could have allowed for some seat leakage.

This, and several minor material discrepancies,

were

addressed

to the licensee.

The inspector assessed

the licensee's

response

to this radiological event to have been good.

Based on the nature and duration of the discharge,

as well as the measured contamination levels,

the inspector assessed

that the radiological significance of this event was minimal.

At the close of the inspection period, the licensee

s root cause investigation was in progress.

The inspector had no further questions at this time.

4.1.3

ALARAPlanning For Outage

The inspector reviewed

the ALARA planning packages

that will be used to support core

offload/refueling operations and motor operated valve testing during the 1994 outage.

Through

this review, the inspector determined that the licensee has proactively addressed

measures

to

reduce

exposure

to personnel

performing these

tasks.

These

measures

included mock-up

training, job site decontamination,

shielding installation, equipment pre-staging,

and work

package/procedure

development.

The inspector

concluded

that these

measures

reflected

attention-to-detail in job planning and preparations to minimize dose.

4.2

Security

4.2.1

Routine Observations

During this inspection

period,

the inspectors

verified that x-ray machines

and metal

and

explosive detectors were operable, protected area and vital area barriers were well maintained,

personnel were properly badged for unescorted or escorted access,

and compensatory

measures

were implemented when necessary.

4.3

Hre Protection

4.3.1

Routine Observations

The inspectors periodically verified the adequacy of combustible material controls and storage

in safety-related areas of the plant, monitored transient fire loads, verified the operability of fire

detection and suppression

systems,

assessed

the condition of fire barriers,

and verified the

adequacy of required compensatory

measures.

No discrepancies

were noted.

10

5.0

SAFETY ASSESSMFAT/QUALITYVERIFICATION

5.1

Periodic Reports

Periodic reports

submitted by the licensee

pursuant

to Technical Specification 6.9.1 were

reviewed.

Inspectors verified that the reports contained information required by the NRC, that

test

results

and/or

supporting

information were

consistent

with design

predictions,and

performance specifications, and that reported information was accurate.

The following reports

were reviewed:

Monthly Operating Reports for January and February 1994

Semi-annual Radioactive Effluent Release Report (July-December

1993)

No unacceptable

conditions were identified.

5.2

Licensee Event Reports

Licensee Event Reports (LERs) submitted to the NRC were reviewed to determine whether

details were clearly reported,

causes

were properly identified, and corrective actions were

appropriate.

The inspectors also assessed

whether potential safety consequences

were properly

evaluated, generic implications were indicated, events warranted additional onsite follow-up, and

applicable requirements of 10 CFR 50.72 were met.

The following LERs were reviewed (Note:

date indicated is event date):

94-001, Radiation Monitor R-32 (Main Steam Line) Not Properly Calibrated.

R-32

output was one decade low due to a technician's mathematical error.

(January 19, 1994)94-002, Containment Pressure Transmitters PT-947/PT-948 Inoperable Due to a Blocked

Sensing Line (February 2, 1994)

The inspector concluded

that LER 94-001 was accurate,

met regulatory requirements,

and

appropriately identified the root causes.

Shortcomings identified in LER 94-002 are addressed

in section 3.2 of this inspection report.

In response,

the licensee willsubmit a supplement to

LER 94-002.

5.3

Nuclear Safety Audit and Review Committee Meeting

On February 24, 1994, the inspector attended a meeting of the Nuclear Safety Audit and Review

Committee.

Topics included review of recent plant events, technical specification improvement

program status, a presentation by the modification subcommittee including discussion of recent

PASS modifications, review of licensee event reports, an outage overview presentation,

and a

review of QA/QC subcommittee activities. The inspector determined that the licensee satisfied

11

the requirements oftechnical specifications 6.5.2 regarding committee membership composition

and quorum.

The inspector concluded that topics were candidly discussed

and were presented

with sufficient detail for board members to assess

the safety significance of the agenda issues.

5.4

Regional Staff/RG&E Management Meeting

On February

17, 1994, RG&E management

met with the NRC staff in the Regional office to

discuss proposed changes to the licensee's Quality Assurance Plan, including implementation of

a peer inspection program.

Additional topics discussed

were 1994 refueling outage plans,

maintenance rule implementation status, and quality improvement initiatives.

Attendees at this

meeting are identified in Attachment I.

Handouts provided by the licensee are included as

Attachment II to this report.

6.0

ADMINISTRATIVE(71707, 30702, 94600)

6.1

Deep Backshift Inspection

During this inspection period,

deep backshift inspections

were conducted

on February 21,

February 27, March 5, and March 6, 1994.

6.2

Exit Meetings

At periodic intervals and at the conclusion of the inspection, meetings were held with senior

station management

to discuss the scope and findings of inspections.

The exit meeting for the

current resident inspection report 50-244/94-05 was held on March 14, 1994.

I

ATTACHMIi22IT1

NAME

REGION I/RG&EMEETING

QA PROGRAM CHANGES AND 1994 REFUELING OUTAGE PLANS

FEBRUARY 17, 1994

TITLE

~R&E

Steven Adams

Charles Anderson

John Cook

Thomas Marlow

Robert McMahon

Joseph Widay

George Wrobel

Superintendent,

Support Services

Manager, QA

Manager, Planning and Scheduling

Manager, Quality Performance

QC Engineer-Operations

Plant Manager-Ginna

Manager, Nuclear Safety &Licensing

Suresh Chaudhary

Allen Johnson

William La2arus

James Linville

Michael Modes

Thomas Moslak

Senior Reactor Engineer, DRS

Project Engineer, NRR

Chief, Reactor Projects Section 3B, DRP

Chief, Projects Branch 3, DRP

Chief, Materials Section, DRS

Senior Resident Inspector, Ginna

ATTACHM<22lT2

REGION I/RG&EMEETING

QA PROGRAM CHANGES AND 1994 REFUELING OUTAGE PLANS

MEETING SLIDES

FEBRUARY 17, 1994

RGckElNRC MEETING

February 17, 1994

nl

J. Widay

5 Min.

li

V if'

nPr

m

~

Purpose

~

Program Description

~

CFR 50.54 Change Basis

Questions/Open

Discussion

S. Adams

5 Min.

C. Anderson

10 Min.

15 Min.

R. McMahon

20 Min.

ali

Im r vmn

ii iv

T. Marlow

15 Min.

IV.

1

4

J. Cook

15 Min.

V.

Mi

l Im lmn

i

S. Adams

15 Min.

QUALITYVERIFICATIONPROGRAM

PUIU'OSE

i

fWr

li h

~

Enhances ownership of work

accomplished

Clarifies accountability of work

~

Enhance pride in workmanship

n

~

Eliminate waiting for inspector

QUALITYVERIFICATION

B

k r

n

~

Quality standards traditionally

assigned to the Quality Control

organization.

~

Maintenance expressed

interest in

performing "quality" verifications.

~

Quality Performance

screening of

selected inspection hold points with

pertinence to ANSI and other

recognized and appropriate

engineering codes and standards.

t

~

Based on importance, complexity, and

training.

QUALITYVERIFICATION

Quality Verification (QV) - Checks or

process monitoring performed and

documented to assure task acceptability by

an individual who is trained and qualified

to perform the task, but did not perform

the task being verified.

QUALIZTVERIFICATION

ifi A

i

i n

'n

quality inspection

quality inspection

quality verification

quality verification

for cleanliness

level B, C 8c D

EXAMPLE

Cleanliness Inspection Procedural Change to

Quality Verification

M- 71

" 'IDi hr

V v

M in

During work planning within the shops if

Quality Control and Maintenance concur

that an existing Quality Control hold point

is for an.ASME Class 2 or 3 component

requiring Cleanliness level B, C or D then

V

'

would be applicable.

step 5.3

LD P

step 5.3.1

JQ.C.

to perform

cleanliness inspection in

accordance with

m/QCIP-5 on all parts prior

to assembly.

ÃrJQC

QUAI.IZTVERIFICATION

Pr nnl

lifi

i n

~A~ri gt;

i

V ifi

N4

2 LvlI

Education

H.S. Graduate or

equivalent

H.S. Graduate or

equivalent

Experience

4 yrs. related plus

qualif. per N18'.1

3 yrs. related or

1 yr. as a Level I

Physical

near vision - annual

color vision - initial

near vision - annual

color vision - initial

Requalification

3 yrs. maximum

3 yrs. maximum

~

Quality Verification requirements

meet or exceed the N45.2.6 Level II

requirements.

1

~

Quality Verifier training includes instructions on duties and

responsibilities of a quality verifier and demonstrated proficiency.

QUALITYVERIFICATIOX

n

n

~

Quality Verifier did not perform the

specific task being verified.

~

Consistent with N45.2 QA Program

requirements

Cl

organizational structure

verification of conformance

~

Effectiveness by QA/QC oversight.

QUALITYVERIFICATION

a

Verifier reports to Line Organization

Documentation of discrepancies.

r

'n

n Tr

in

~

Assessment

results willbe tabulated

and trended by QC.

Discrepancies willbe tracked by

Maintenance.

QUALIZTVERlFICATION

L

T

Selection of activities

Define Quality Verification

Interview line organization

Presentation of program to GPC and endorsement

OS/01/93

Completed

12/13/93

Completed

12/15/93

Completed

01/07/94

Completed

Presentation of program to Maintenance and

endorsement

01/07/94

Completed

Write and approve implementing Administrative

procedure

Write.and approve guidelines that direct torquing

and cleanliness

01/14/94

Completed

01/28/94

Completed

Provide an assessment

plant of QV during the

94 Outage

Approval of changes

to A-503 & A-1603.3

Revision to QAM Sect. 10 and Glossary

10CFR50.54 Analysis

Revise QCIP-1 gnspection Instructions)

NRC introduction meeting to QV

Training of Maintenance personnel

02/01/94

Completed

02/02/94

Completed

02/07/94

Completed

02/10/94

Completed

02/15/94

02/17/94

02/28/94

QUALIZYVERIFICATION

vri h

~

QA/QC personnel

a

Sample plan

~

Specific criteria assessed

a

Week1y progress meetings

'

Updates to NAM and Line

Management

Final Assessment

r

10 CFR 50.54 CHANGE BASIS,

Impact on Traditional QC Inspection

Scope Limited - routine, repetitive

tasks

~

Complexity Modest - witness, check

~

QC Involvement Remains Extensive

CONSISTENCY WITH

ANSI/IEEE/APPENDIXB

Standards

recognize requirement

variability e.g. N45.2.8

~

Screening criteria based on variability

for:

Cl

Risk

C3

Complexity

C3

Inspector Training

~

QV selections consistent with criteria

~

QV approach - consistent with

Appendix B, II (control extent

consistent with Importance to Safety)

T

N - Comparison of Control

(Quality Inspection vs Quality Verification)

D - Similarity

~

Attribute definition

~

Acceptance Criteria Specified

~

Education and Experience

~

Structured Training

Demonstrated Proficiency

Near and Color Vision

~

Qualification Documented

Verifier not responsible

~

QA/QC Oversight

~p

h

UNCHANGED ELEMENTS

.

~

Total QC/QV Hold Points Unchanged

~

Quality Inspections remain QC

cognizance

~

QV - Independent Verification

Similarity

SUMMARYAND CONCLUSION

Personnel qualifications

~

Independence

~

QA/QC Oversight

Ginna Safety and Reliability Enhanced

Coimnitments Not Reduced

RG&E/NRC REGIONIMEETING

February

17, 1994

i n

I

n

iI

n

r n

r

Rviin

r Dir

i

i Pr

m rhniv

mn

V.

r R

w

1

1

1

i

n in

D

m n

In rf

li

n-I.in R vi

VIII.

R

'

Quality 'Provement initiative Milestones

Attachment

2

Nuclear Directives

Prograa Aevision:

Expand

QA Scope

Change to VP trow Sr.

VP

Reduce In-Line Reviews

P-8 Audit Frequency

Work by Directives

QA Manual Phase

Out

Reforest por SRP 17.3

) 994

Develop/Approve

Develop/Approve/Subait

NAC Approval

or 60 days

Iepl scent

1996

Annual

FSAA Update

VP chango

Align w/prograw

Develop

QA Grading

QV Prograa

Prepare/Subait

Develop, Train

Iapleaent

Asview, Expand as appropriate

Reduce In-Line Reviews

Coaproheneive

Assessments

Tech Spec Revision

Aeviso Section

S.O

Interia Prograw Revision

Audit Frequency

Prepare/

a t

Iwploaont

Iapleaent

MC Approval

leplseent

NRC Approval or 60

days

lnteria Prograw Aovision

Procedure

Review Por iodicity

prepare/

Subwit

legis aent

QUALIZTASSURANCE PROGRAM

FOR STATION OPERATION

QAPSO REVISION

1

f

P17

Ar

C3

Management

0

Performance

0

Assessment

r

IP ni i iv

GINNA NUCLEAR DIRECTIVES

~

Contain Existing Appendix B

QA Criteria

~

Nuclear Directives WillReplace

QA Manual

~

Ownership of QA Policy/Directives

by Vice-President

~

Corporate Responsibility for:QA

Program Shifting from Senior Vice-

President to Vice-President

~

Willbe Included in QA Program

Submittal, End of 1994

L

COMPREHENSIVE ASSESSMENTS

a

.

Performance Based Assessments

Transition to Proactive Oversight

versus Mandated Audits

~

Determine Assessment

Scope and

Process

Cl

Effective Scoring System

0

Areas of Concentration

Cl

Past Performance Dictates

Priority, Frequency, Importance,

History

Overall Results Determine Need for

Audit

PROCEDURE

REVIEW'ERIODICIZY

~

Symptom Based, Event Driven

Procedure Review Will Continue

~

Reviews Replaced With Programmatic

Controls Based Upon Procedure

Usage and Alternative Procedure

Control Programs

Periodic Review Requirements for

Certain Procedures

Deleted

El

Administrative

C3

Technical

.1I

~

.

T

Y

E

t

LICENSINGDOCUMENTS INTERFACE

a

Plans to Upgrade to Improved Technical Specifications

Evaluate Administrative Controls Section 6.0 of Existing T.S.

Section

6.5.1

PORC

6.5.2

NSARB

Description

Relocate/Change

Relocate to QA, or UFSAR

Emergency,

and Security

Programs

Relocate to QA, or UFSAR

Emergency,

and Security

Programs

6.8

Procedures

Relocate review and approval

process of procedure changes

to QA Program or UFSAR.

6.10

Record Retention

Relocate to QA Program or

UFSAR

~

Relocation of changes to UFSAR would be submitted to NRR along

with TS Amendment

~

Relocation to QAPSO willrequire interim submittal (March)

~

Potential mid-year QAPSO submittal - procedure review

End of year major revision to QAPSO.

~

UFSAR Chapter 17 willcontain QAPSO

~

Changes required to Chapter 13 of UFSAR

QUALIZTIN-LINEREVIEW

.

PHASE OUT

~

Establish Transfer Plans

Cl

Procedures

Cl

Approvals

CI

Training

Cl

Define Oversight Methodologies

Transfer Processes

to Line

Organizations

Implement Oversight

Discontinue Low Value-Added

Reviews

Grading of QA Requirements

.

r Ini i iv

1

i

Cl

Documentation

0

Control

Cl

Verification

1 -

h

1

i

ff

AllSteps

Verifications

Hold Points

N/A

Yes

N/A

Final Signor

N/A

N/A

N/A

Final Signoff

- QUALITYVERIFICATION .

FUTURE PLANS

Goal is to maximize worker

responsibility for quality while

assuring optimum utilization of

resources.

~

Three year program to integrate

traditional QC into line organizations.

~

Existing QC personnel transferred into

Operating Departments.

Department personnel trained and

qualified to same standards

as present

QC personnel.

~

Results reporting shifted to line

organizations.

1994 OUTAGE PRESENTATION

mn lni

i IP

n I

1994 OUTAGE OBJECTIVE

.

RGRE

TE

ORK

SAFETY

QUALITY

SCHEDULE

INNA STA110h

.

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<<9!tPIARY DARCHAR~

tlARCH

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5

5

5

5

tl

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5

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5

5

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8

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5

5

?

6

9

13

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l2

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IA

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22

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21

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I

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5

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26

29

30

31

2

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2

3

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FILL I ILRI R 'SIFLC 'AR":- IL I III,

BAPR9A

I

OUTAGE

PERFORMANCE

INDICATORS

QFETY

!~

1993

GOAL

1993

ACTUAL

1994

GOAL

~ 1994

BUSINESS

PLAN

Lost

Time

Accidents

0

0

0

0

Person-Rem

Ex osure

Contaminations

Rad

Waste

Generation

210

155

140

140

96

100

1000

cu.

980

cu.

900

cu.

ft/wk

ft/wk

ft/wk

190

130

9,000

QIJAL1TY.

Preventive

Maintenance

Corrective

Maintenance

Ins ections

Rework

9096

9096

90%

96. 4%

93.896

99. 196

0.9%

9596

9596

9596

!,! 'EGUL'ATORY " I~

"

License

Event

Re orts

(LERs)

HRC

Si

ificant

Events

0

0

0

0

PI ANT

IMPRQVEMENTS

~

Modification

Work

90%

10096

95%

OPERABILITY

Startu

Problems

Continuous

Run

0

60

60

0

60

~i ~

CORPORATg

. e e~

Outa

e

Len

h

55

45.3

39

49

RF/kal:outper94.ind

1994 AI.AO OVERVIEW

V

1

Defueling

HP Turbine Minor Inspection and

Preseparator

Pipe Wall Repair

PORV Refurbishment

A RCP Seal Inspection

A RCP Motor Swap

Service Water Outage of A and B

Loops

C3

Valve

Replacement/Ref'urbishment

C3

A Service Water Header

Inspection

1&4 AIck0 OVERVIEW

iv'

(cont'd)

~

Refurbishment of 101XU's

C3

Service Water

0

CCW

Primary Side Valve Inspection

0

CV 842 A8cB

El

CV 867 AAB

~

S/6 Inspection and Repair

I

a

Rod Control System Card

Replacements

8c Minor Modifications

Rx Compartment and Bus Duct

Cooler Replacement

¹ Work Orders Planned for Outage

C3

IA,C

338

CI

Mechanics

118

Cl

Pipe

276

C3

HVAC

49

CI

Electricians

TOTAL

928

OUTAGE RISE MANAGEMENT

Use of PRA to Evaluate Outage

Configuration

Delayed Installation of S/G Nozzle

Dams Until After Defueling

~

Improve PORC Overview of Outage

Activities

~

Fire Protection Review of Outage

Activities

Added NSL Personnel to Outage

Safety Assessment

Team

GINNA STATION

MAPPFENANCE RULE IMPLEMENTATION

Current Status

II.

Training

Peer Group Involvement

Project Team Composition

V.

Major Milestone Schedule

Reorganization in November to

dedicate one Manager full time to

Maintenance Rule implementation

efforts.

Project Team formed - 1st

meeting 2/10/94

~

EOP review for "Non-Safety

SSCs in EOPs" in progress

(Operations)

80 key players briefed (10 sessions)

including

~

(Company-Wide) 31 affected

Mgrs 8c key supervisory

personnel

~

System Engineers

~

Operations (4 of 6 shifts)

Craft training planned after

project completion

a

Westinghouse Two Loop Group

~

MR Info. Sharing Committee

. Mtg. (NMPl,"NMP2,

Fitzpatrick, Ginna)

a

Region

1 Utilities

Project Manager

John Fischer, Director Maintenance Rule

Design Engineering

Len Sucheski, Supervisor, Structural Engineering

Instrumentation 8c Control and Electrical

Robert Popp, INC/Electrical Station Engineer

Materials Engineering 8c Inspection Services

Frank Klepacki, ISI Engineer

Nuclear Safety Sc Licensing (Programs)

David Wilson, Associate Engineer

Nuclear Safety 8c Licensing (License Renewal)

John Jorgensen,

Senior Nuclear Engineer

Operating Experience

Frank Puddu, Operating Experience Specialist

rl

jl

'J

'I

n(

(cont'd)

Operations

Doug Peterson,

Operations-Maintenance

Liaison

(Shift Supervisor)

Preventive 4, Predictive Maint./RCM/NPRDS/Root

Cause Analysis

Tom Plantz, Maintenance Systems Manager

Performance Testing

Gregg Joss, Results 4, Test Supervisor

Scheduling

John Cook, Planning 8c Scheduling Manager

System Engineers 4 Modifications

Jeff Wayland, Lead Engineer - Systems Engineering

Sub stations

Terry Walter, Manager, System Design Engineering

Jeffrey I'iske, Supervisor, Substation Design

V.

2/94

5/94

6/94

10/94

Majority of the data

gathering in place

Complete MR scoping

Determine risk significance

Identify affected processes

J

AllSSC performance

criteria complete

Allaffected processes

modified

4Q94

4Q94

IQ95

7/95

7/96

C assist visit

RG8cE QA Audit

NRC non-enforceable

inspection

RGB Goal MR

Implementation Deadline

10CFR50.65 Legal MR

Implementation Deadline

H

>l