ML17187B032

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Insp Repts 50-237/97-07 & 50-249/97-07 on 970414-0512. Violations Noted.Major Areas Inspected:Licensee Maint, Engineering & Plant Support
ML17187B032
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 06/05/1997
From: Caniano R, Hiland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17187B030 List:
References
50-237-97-07, 50-237-97-7, 50-249-97-07, 50-249-97-7, NUDOCS 9706270328
Download: ML17187B032 (52)


See also: IR 05000237/1997007

Text

U.S. NUCLEAR REGULA TORY COMMISSION

Docket Nos:

License Nos:

Report No:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Submitted By:

Approved By:

9706270328 970613

PDR

ADOCK 05000237

G

PDR

REGION Ill

50-237; 50-249

DPR-19; DPR-25

50-237197007; 50-249/97007

Commonwealth Edison Company

Dresden Nuclear Station Units 2 and 3

Opus West Ill

1400 Opus Place - Suite 300

Downers Grove, IL 60515

April 14 through May 12, 1997

M. Farber, Reactor Inspector, Riii

B. Bartlett, Senior Resident Inspector, Riii

K. Riemer, Senior Resident Inspector, Riii

R. Paul, Senior Health Physics Inspector, Riii

C. Johnson, Reactor Inspector, RIV

F. Gee, Reactor Inspector, NRR

C. Settles, Inspector, Illinois Department of Nuclear

/3'1 /~ C/f/q7

P. L. Hiland, Chief, Fuel Cycles Branch,

Team Leader, Division of Nuclear Material Safety, Riii

a~c:~~~ 7!"/s-/7? .

J

aniano, Acting Director,

.

Manager, Division of Nuclear Material Safety, Riii

EXECUTIVE SUMMARY

Dresden Nuclear Station Units 2 and 3

NRC Inspection Report 50-237197007; 50-249/97007

This special safety maintenance team inspection included aspects of licensee maintenance,

engineering, and plant support. The report covered a 2-week onsite period of inspection

by the full team, and some onsite followup inspections conducted by individual team

members up to the date of the exit meeting held on May 12, 1997.

Maintenance Program

Work Control

The outage control center (OCC) functioned adequately and was providing the services

expected from it. Personnel staffing the OCC understood their positions and objectives,

and were generally supporting the outage adequately. With one unit in a refuel outage and

a second unit in a forced outage, coordination problems between the Unit 2 and Unit 3

outage organizations were initially observed early in the inspection; however, corrective

actions by the licensee significantly reduced the coordination problems over the 2-week

onsite inspection period.

The work execution center (WEC), located just outside the main control room, was

functioning effectively in reviewing and approving work packages and meeting the

objective of reducing control room operator distractions. However; uncontrolled

documents (desk top instructions) were being used in the WEC and elsewhere to enhance

existing approved procedures. The team considered the licensee's approach to resolution

of this issue acceptable.

The performance of work analysts was adequate, and work packages reviewed were

generally of good quality. The work package rejection rate, while not precisely fixed, was

not excessive. However, the work analysts were called upon to perform tasks which

would normally be considered engineering. Examples included parts evaluation and system

interaction analysis.

The original Unit 2 forced outage schedule was prepared to address three major problems:

the switch block cracks in Merlin-Garin 4kV breakers, leaking "X-area" coolers, and a

condenser tube leak. Each of these activities exhibited elements of inadequate planning or

coordination problems.

The licensee's existing and future scheduling systems appeared to be well thought out and

structured. With Unit 2 in a forced outage and the new program in the early stages of

implementation, an historical review was not conducted and no assessment was made

with regard to the effectiveness of either the 12-week or 5-week programs (rolling

schedules).

2

,J

.. ,

Two violations, with two examples each, were identified regarding the failure to follow

station administrative and surveillance test procedures. In the first example (M3.1 ),

station administrative procedures were not followed to obtain a controlled key, and in the

second example (M3.2), the station's approved method for independent verification was

not translated into the implementing instructions. In addition, the training of contract

Instrument Maintenance Department (IMO) technicians regarding the requirements of

independent verification was not consistent with other maintenance departments.

The third and fourth examples (M4.1) of a violation in this area involved failure to follow

test instructions. In one example, a power supply was left energized following testing

contrary to procedural direction, and the other example involved using a wrong procedure

.revision to perform testing .

Mechanical Maintenance Performance

Mechanical maintenance activities were generally well performed. However, a violation

with three examples of failure to follow station administrative requirements to assure

proper foreign material exclusion were identified (M4.2). A separate violation (M4.2) with

two examples was identified for failure to follow specific mechanical maintenance work

instructions. The first example was a failure to monitor weld interpass temperature, and

the second example involved performance of work without a sufficient work package at

the job site. In addition, some poor work practices were identified with regard to minimum

protective clothing requirements and unapproved rigging of components to piping systems.

Electrical Maintenance Performance

In general, electrical maintenance was properly planned, performed, and documented.

Workers were knowledgeable and capable of performing the assigned work activities.

Work observed in the switchyard was appropriately controlled and conducted in a manner

to minimize the possibility of an offsite power interruption. Field work was effective at

installing an emergent 4kV breaker modification, and assigned personnel appropriately

halted work when discrepancies were noted in the work package instructions.

Two violations (M4.3) regarding the conduct of a Unit 3 "modified performance discharge

test" for the 250 voe battery were identified. First, test personnel failed to comply with a

Technical Specification surveillance requirement to test in the "as found" condition.

Second, a corporate engineering memorandum, recommending testing the 250 voe

3

..

battery in other than the uas found" condition, was not evaluated in accordance with the

station's processes for procedural changes. The battery surveillance test problems

appeared isolated, but the ident,ified problems were significant with respect to test

procedural control, quality, and performance.

Maintenance Backlog

The action request (AR) backlog was relatively low and only contained tasks that would

not require a station work request to accomplish. The non-outage work request backlog

contained tasks that were appropriate to be worked while the units were operating. The

outage work request tasks were appropriately assigned to work during a unit outage. In

addition, reasonable explanations were provided for work tasks deferred to future outages.

Knowledge of the current maintenance backlog was good. In general, the maintenance

backlog was appropriately coded. so individuals responsible for work prioritization had a

sound data base. Some confusion existed in the data base due to incorrectly coded work

requests and work tasks that were included in the data base, but actual field work was no

longer required. The backlog of non-outage work request tasks was skewed in a direction

indicating positive progress was being made at reducing the oldest backlog items and

focusing attention on more recent equipment deficiencies.

Plant Support

Radiological Protection Performance

Some corrective actions to improve the control of licensed radioactive material within the

site's radiological protected areas (RPAs) have been adequately implemented. Actions

. scheduled for implementation after the current Unit 3 outage appeared sufficient to

improve licensee performance in this area. However, some training and repair issues

remained incomplete. In addition, the action to have the greeters address HRA issues was

not communicated to the greeters, and was not being conducted.

In general, radiological controls, ALARA initiatives, and job planning were effectively

implemented which contributed to the lower than projected dose for the outage to date.

Although some poor radiological work practices were observed, overall, there was good

effort to prevent loitering and unnecessary crew size.

One example (R 1.4) of a procedural violation regarding radiation worker practices was

identified for failure to wear personal dosimetry in accordance with station administrative

requirements. In addition, weaknesses were identified concerning poor housekeeping

practices.

4

REPORT DETAILS

Summary of Plant Status

Unit 3 was in the third week of a scheduled refueling outage. On April 11, 1997, three

days prior to the start of the inspection, Unit 2 entered a forced outage to repair cracked

switch blocks on safety-related 4kV Merlin-Garin circuit breakers. Both units remained in

outages throughout the inspection period.

I. MAINTENANCE

M1

Conduct of Maintenance

M 1 .1 Work Control

a.

lnsoection Scope

(

The team examined the procedures and processes associated with outage work

control. The team also monitored activities in specially designated outage

management work spaces.

b.1

Observations and Findings on Work Execution Center

The team reviewed the work execution center (WEC) instructions, interviewed WEC

staff, and monitored WEC activities. The WEC was responsible for authorizing the

conduct of work after assuring work package completeness, out-of-service

placement, and schedule adherence. The intent of the WEC was to reduce the

amount of traffic in the control room, thereby reducing control room operator

distractions. The WEC staff consisted of a supervisor, window coordinator, Unit 2

and 3 field supervisors, and an out-of-service (00S) supervisor. The WEC staff

were knowledgeable regarding the electronic work control system (EWCS), OOS

procedures, plant conditions, and outage schedules. The team observed the

processing and approval of work packages for replacement of brushes on both of

the Unit 2 recirculation pump motor-generators. The window coordinator reviewed

the packages and concluded that the contents were acceptable and met the

requirements of Dresden Administrative Procedure (OAP) 15-06, "Preparation,

Approval, and Control of Work Packages and Work Requests." The coordinator

also verified that the OOS had been placed and that the work gro1.,.1p supervisor was * *

signed on to the OOS.

The team reviewed the WEC instruction binder. The instruction binder consisted of

16 instructions and 2 notes which provided guidance on a variety of topics such as

valve and electrical lineup control, COS package control, procedure revision review,

pre-authorization of work packages, and electrical bus outage generic guidelines.

5

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c.1

b.2

The team noted that most of these instructions dealt with operation of the WEC.

However, in several cases, the instructions served as clarifications or detailed

guidance for implementation of approved procedures. Of note were instructions

concerning lineup and OOS package control, pre-authorization of work packages,

and electrical bus and motor control center outage generic guidelines. WEC

instructions were not reviewed, approved, or controlled. Use of uncontrolled

guidance for the implementation of approved procedures was also noted in the

work package preparation area and is discussed in Paragraph M1 .2.b.1.

Conclusions on Work Execution Center

The team concluded that the WEC was functioning effectively in reviewing and

approving work packages and meeting the objective of reducing control room

operator distractions.

Observations and Findings on Outage Control Center

The licensee elected to establish independent outage management organizations to

handle the Unit 2 forced outage concurrently with the Unit 3 refueling outage. The

licensee also elected to keep maintenance resources separated between the outage

organizations. The team monitored the operation of the Unit 2 forced outage "mini-

outage control center (OCC)," and the Unit 3 refueling outage OCC. During this

monitoring the team examined the functions of the positions established in the

OCC: the shift outage manager, the maintenance outage manager, the plant

support manager, and the outage risk manager. Members of the licensee's staff

filling these positions were interviewed to assess their understanding of outage

management and the processes involved. The team also consistently attended

regularly scheduled outage management meetings to evaluate coordination between

station departments and between Unit 2 and 3 outage management organizations.

While the licensee's decision to establish separate outage organizations was

fundamentally sound, problems were encountered in implementing this approach

early in the Unit 2 forced outage. The problems appeared to emerge from the rigid

approach to keeping maintenance resources separated. Most of the station's

maintenance resources were designated for the Unit 3 refueling outage with the

expectation that Unit 2 would remain in operation. A short outage schedule was in

place as required by OAP 18-02, "Unscheduled Force.d or Maintenance Outage

Planni.ng." However, there were no indications of any planning to provide resources

to implement that schedule in the event of a Unit 2 forced outage. Consequently,

when Unit 2 was shut down, adequate resources were not available to deal with

the scheduled work activities. Shortages were immediately evident in all

disciplines, most nqtably carpenters for scaffolding construction and radiation

protection (RP) technicians for area surveys. To immediately address the problem

RP technicians were pulled from Dresden Unit 1 and the craft assigned to the fix it

now (FIN) team were reassigned to Unit 2. Difficulties obtaining carpenters for

scaffold erection continued through Tuesday, April 1 5, until the two outage

managers met and developed a policy for sharing carpenters and other resources.

This was one example where outage coordination was initially ineffective.

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{'

...

Early in the Unit 2 forced outage, it was recognized that two new "X-area"

[outboard main steam isolation valve room] coolers would not be onsite in time to

support the Unit 2 scheduled startup date. A decision was made to transfer a

cooler from the Unit 3 X-area. During a subsequent meeting on April 17, the topic

of which Unit 3 cooler was to be put in Unit 2 was discussed and outage staff

present at the meeting were unaware that the decision had been made, nor was the

outage staff aware of which cooler had been selected. That was another example

of ineffective coordination.

A major activity during the Unit 2 forced outage was to identify and repair a

condenser tube leak in the north water box. Coordination problems were evident

early on with problems in obtaining qualified individuals to erect scaffold, conduct

radiation and contamination surveys, and conduct confined space surveys. These

problems, along with the planning problems discussed in Section M1 .2.b.2,

impeded the job until a designated team with a project manager was *established.

After this team was established and a detailed schedule was prepared, condenser

repair activities proceeded more effectively. This was an additional example of

ineffective coordination.

Initial coordination problems between the two outage management organizations

were due, in part, to a lack of participation by the respective staffs in meetings held

by the other outage staff. The first day of the inspection the team noted that no

staff from the Unit .2 outage organization was present at the 6:30 a.m. Unit 3

outage status meeting, nor were staff from the Unit 3 outage organization present

at the 7:30 a.m. Unit 2 outage status meeting. The situation was identical atthe

1 :30 p.m. and 2:00 p.m. outage schedule review meetings. This was corrected the

next day and although some lapses occurred over the next few days, cross-

participation became routine and effective in identifying issues _with potential

overlap.

During the review of the outage organizations, the team found that the positions

established for the Unit 3 refueling outage were appropriate for dealing with the

major areas of outage management. For example, the plant support manager was

responsible for engineering and other plant support departments. The maintenance

outage manager was responsible for overseeing job status and resolving problems

identified by the work groups. The outage risk manager was responsible for

monitoring shutdown risk status and ensuring that shutdown risk assessments

were performed periodically and when required for changes in plant configuration.

This activity was especially important during the electrical lineup changes that were

necessary to support the 4kV breaker repairs. The shift outage manager was

responsible to the station manager for overall outage performance and monitored

schedule and budget performance, coordinated the efforts of the other outage

managers, responded to emergent issues, and coordinated resources and activities

with the Unit 2 outage manager. The Unit 2 forced outage organization was similar

in concept, but was not staffed as comprehensively. The team noted that the

individuals staffing these positions in both outage organizations understood the

assignments and the station's outage management program.

7

-(.

During the early part of the inspection, the team noted that regularly scheduled

meetings intended to either review outage status or examine the schedule were

generally unstructured, informal, unfocused, and did not address specific

accountability for assigned tasks. As the first week of the dual unit outage

progressed, the team noted changes in these meetings. The meetings became

more business-like and formal, discussions focused on specific tasks, individuals

were assigned to specific tasks, and accountability for completion was exacted.

This transition began with the Unit 2 outage meetings and by the beginning of the

second week, was occurring with the Unit 3 outage meetings.

  • c.2

Conclusions on Outage Control Center

The team concluded that the OCC was functioning adequately and that it provided

the services that licensee management expected of it. Personnel staffing the OCC

understood the assigned positions, the objectives, and were generally supporting

the outage adequately. Coordination problems between the two outage

organizations were identified early in the first week of the inspection; licensee

corrective actions subsequently reduced the occurrence of these problems. The

team also concluded that there was a need to sharpen the focus of regularly

scheduled meetings.

M1 .2 Planning and Scheduling

a.

lnsoection Scope

The team reviewed the procedures and processes associated with planning and

scheduling, including work package preparation, individual task plans, and

scheduling systems used by the licensee. The team also assessed the licensee's

ability to maintain the established schedule. The team interviewed members of the

licensee's staff involved in the planning and scheduling processes. The team also

reviewed the new corporate-wide non-outage scheduling system which Dresden

was just beginning to implement.

b. 1

Observations and Findings on Work Package Preparation

The team reviewed OAP 15-06, *preparation, Approval, and Control of Work

Packages and Work Requests," Work Analyst Guide to Work Package Preparation,

EWCS Desk Top Instructions, and Maintenance Department Memo No. 100.14,

Dated August 30, 1996. In addition, the team reviewed the following work request

(WR) packages:

WR 960105540-01.

WR 970041990-01

U2 HPCI [high pressure coolant injection] Pump Suction

from Condensate Storage Tank Check Valve

Disassembly and Inspection

U2/3 Air Filtration Unit 4-lnch Charcoal Filter Halide

Testing

8

WR 950060862-01

WR 950065566-01

WR 960099060-01

WR 970044365-01

Bus 34 - Clean, Inspect Bus Bars, Wiring, Supports,

Insulation .

U3 Main Steam Line C High Flow Isolation Non-TS

Surveillances

Install Terminal Screws to A TWS [anticipated transient

without scram] Analog Trip System Cabinet A

Reinforce U2 Flued Head Anchor X-116B

No deficiencies were identified with any of the six packages

The team interviewed a work analyst and observed the preparation of a work

package for replacement of a solenoid valve on the Unit 2 high pressure turbine.

The team noted that the analyst was responsible for parts research, detailed work

instructions, radiation work permit (RWP) preparation, and evaluation of system or

component interactions and impacts. The analyst indicated that the majority of

time spent in package preparation was related to parts research, selection, and

justification. Considerable time was also expended in the research and

development of detailed work instructions. The station did not maintain a

comprehensive set of approved maintenance work instructions, consequently the

analysts were frequently required to provide detailed work instructions. The analyst

was also required to perform an impact analysis which examined the system

interfaces and interactions to identify possible alarms, actuations and interferences.

The analyst was familiar with the EWCS and the various data bases available and

consequently did not need to use the work analyst guide nor the desk top *

instructions (OTI). The analyst indicated that these guidelines were available and

were used extensively by recently assigned analysts still gaining familiarity with the

process.

The team reviewed both the work analyst guide and the OTls and noted that neither

of these documents were reviewed, approved, or* officially controlled. A pseudo

control (tracking copies) had been applied to the work analyst guide but was

unsuccessfUI. Three copies of the OTls were reviewed in the WEC; one was noted

to have hand-written revisions entered into it. This copy was immediately removed

by the WEC supervisor. The licensee had recognized the potential problems

intrinsic in allowing uncontrolled guidelines to be used to support implementation of *

approved procedures. A nuclear tracking system item had been previously opened

by the licensee to track resolution of this problem. The licensee reviewed the WEC

instructions, work analyst guide, and OTls and concluded that these guidelines had

not been used in the implementation of safety-related processes but recognized the

potential. The licensee committed to revise OAP 09-01, "Station Procedures," to

provide a clear definition for desktop instructions. The licensee also committed to

have working departments review the desktop instructions and initiate changes to

proceduralize the instructions as necessary.

9

Given the lack of comprehensive maintenance work instructions and the

consequent need for generating detailed work instructions, the team was concerned

with the potential for incorrect work instructions reaching the field. The team met

with work analyst supervision and reviewed statistics on packages returned to the

analyst. It was noted that packages were returned to the analyst for a variety of

reasons, most having nothing to do with errors in package preparation by the

analyst. Further discussions with work analyst supervision revealed that there was

no method for discriminating between reasons, no way to directly identify trends

from this data, and no way to determine what percentage of returned packages

were due to preparation errors. There was trending of parts problems, OOS

problems, and RWP problems from other data, but there was no direct correlation

between the two measurements.

The team noted that the work analyst organization had implemented a work

package quality control form in a effort to solicit feedback on the quality of work

packages. The form was not a station requirement; however, the intent was to

provide feedback from the shops after work packages were walked down. The

team noted that for the majority of work packages completed, the form had not

been completed nor was there any feedback on the quality of the package. As

such little or no benefit was being derived from the effort.

c.1

Conclusions on Work Package Preparation

The team concluded that work analysts were performing adequately; work

packages were generally of good quality and that the rejection rate, while not

precisely fixed, was not excessive. The team noted that during package*

preparation, the work* analysts were called upon to perform tasks which would

normally be considered engineering. Examples included parts evaluation and

system interaction analysis. The team also identified that a system of uncontrolled

documents was being used to enhance existing approved procedures. The team

concluded the licensee's existing approach to resolution of the uncontrolled

document to be reasonable.

b.2

Observations and Findings on Work Planning

The team reviewed plans for the three major work activities scheduled for the

Unit 2 forced outage and compared th.em to the actual performance of the work.

These comparisons revealed lapses in the licensee's planning process for each of

these tasks.

The licensee shut down Dresden Unit 2 after identifying that safety-related Merlin-

Gerin 4kV circuit breakers in both units had auxiliary switch blocks that were

cracked. A temporary modification was developed by engineering to correct the

problem. Planning to install this temporary modification included development of a

detailed "fragnet" to sequence the repairs to each breaker. It become apparent

early in the job that the plan had not properly considered all of the changes to the

electrical configurations of both units necessary to support the work. Major bus

outages were considered but other electrical lineup changes were not identified.

10

This resulted in frequent adhoc meetings between outage management and

operations to identify needed configurations, when, and how to get the plant into

those conditions. One example of the impact of this lapse was observed when a

bus drop would have deenergized the power for a diver's air compressor. This was

recognized just before the bus drop was to have taken place. The licensee

subsequently stopped work activities on this job and wrote a problem identification

form (PIF) to evaluate the problem. At the close of the inspection, the PIF was still

in process.

Planning for the Unit 2 condenser tube leak repair was also deficient. A specifically

responsible individual had not been designated, a detailed fragnet to identify the

sequence of activities had not been prepared, mainte_nance technicians had not

been trained on the use of the sonic "gun," the foam needed to confirm the leaking

tubes identified by the sonic gun had not been obtained, and the placing of OOS

and drawing a vacuum by operations were not well coordinated. The job faltered

until a dedicated team with a responsible project manager was selected. At that

point, a detailed fragnet was developed and the job began to move forward. Within

two days after the team was formed, the job was progressing efficiently.

Planning for the "X-area" cooler replacements did not consider the impacts on

Unit 3 nor did it establish which coolers should be transferred between the units.

This lapse was recognized by the Unit 2 outage staff and was resolved before it

impacted the job.

c.2

Conclusions on Work Planning

Initially, the forced outage schedule was prepared to address three major problems:

the switch block cracks in Merlin-Garin 4kV breakers, leaking "X-area" coolers, and

a condenser tube leak. Each of these activities exhibited elements of inadequate

planning or coordination problems.

b.3

Observations and Findings on Non-outage Scheduling

The team reviewed OAP 15-01, "Initiating and Processing a Work Request," OAP

04-02, "Dresden Preventive Maintenance Program Control," Nuclear Station Work

-Procedure (NSWP)-WM-08, "Action Request Screening Process," and NSWP-WM-

09, "Maintenance Work Scheduling Process Week E-5 to E + 1." The team also

reviewed schedules and reports associated with the non-outage scheduling process.

At the time of the inspection, the Dresden scheduling process was a 12-week,

system window program. System windows were scheduled in advance and as

work activities were identified they were assigned to the appropriate window. The

process began 12 weeks in advance of the date of work execution and contained

established milestones for preparation throughout the period. Reports and

schedules were published* periodically throughout the process to track progress.

The process was comprehensive and well:-structured; however, the team was not

able to assess its effectiveness because Unit 2 entered a forced outage on April 11 ,

1997r, three days before the inspection began .

11

c.3

b.4

The team also met with cognizant licensee staff to review and discuss a new

scheduling system commonly known as the "Braidwood initiative." This process

was defined in NSWP-WM-09 and focused on a period encompassing the five

weeks prior to the scheduled work execution to one week after scheduled

execution. As with the 1 2-week plan, there were established milestones for work

preparation. The licensee planned to integrate this new program into the current

12-week cycle and then phase out tracking the actions which took place between

weeks 12 and 5. Those actions would not be eliminated, but work preparation

would be expected to be at the same status when it entered the five-week schedule

as if it had tracked through the process from week 12 to week 5. Because the

program was in the early stages of implementation, the team had no opportunity to

evaluate the system's effectiveness.

Conclusions on Non-outage Scheduling

The licensee's present and future scheduling systems appeared to be well thought-

out and structured. With Unit 2 in a forced outage and a new program in the early

stages of implementation, the team chose to forego a historical review and focus

on activities in process. Consequently the team drew no conclusions with regard to

the effectiveness of either the 12-week or five-week programs.

Observations on Outage Scheduling

The team reviewed OAP 18-02, "Unscheduled Forced or Maintenance Outage

Planning," and OAP 18-04, "Management of Planned Outages." Both procedures*

were comprehensive and appeared to properly address the significant aspects of

outage planning. The team reviewed the licensee's outage scheduling program and

noted that it was essentially a standard P2 process, similar to that used by many

other utilities. The team reviewed several different versions of the licensee's

outage schedules and noted that durations and resource allocation were generally

appropriate. The team noted that the licensee's ability to execute the schedule was

hampered by several factors. Emergent work was the primary factor, as evidenced

by the need to respond to flued head anchor repairs on Unit 2 penetrations X-1168,

X-1098, X-115A, and X-111A, excessive vibration problems with a Unit 3 core

spray pump motor, and failure of a special control rod handling tool, which occurred

during blade swaps. In the latter case, the failure of the control rod tool led to a

licensee investigation and directly caused an hour-for-hour critical path loss. Other

factors which impacted the station's ability to work the schedule could be

collectively described as coordination issues. These included out-of-service

placement problems, parts availability, and overlap between jobs .in the same

physical location. Finally, resources appeared to impact schedule adherence. This

problem was the direct result of the Unit 2 forced shutdown. Because the station

had not planned how to staff a Unit 2 work force in the event of a possible dual-

unit shutdown, maintenance and plant support personnel were assigned Unit 3

tasks, and sufficient personnel were not readily available to perform Unit 2 tasks.

Where Unit 2 tasks had clear priority, resources were diverted from Unit 3

activities, which slowed down the Unit 3 activities. The situation was not expected

to be resolved until Unit 2 returned to power operation.

12

c.4

Conclusions on Outage Scheduling

The team concluded that the station's outage scheduling process was adequate but

that emergent work, coordination problems, and resource problems caused by not

planning how to staff a Unit 2 outage work force impacted schedule adherence.

M2

Maintenance and Material Condition of Facilities and Equipment

M2. 1 General Plant Conditions

a.

Inspection Scope (71707)

The team toured both Units 2 and 3 and observed maintenance and material

condition of plant facilities and equipment. Some of the areas observed were:

  • Unit 3 drywall
  • Unit 2 and 3 turbine deck
  • Unit 3 *refueling deck
  • Unit 2 and 3 HPCl/LPCl/Core Spray rooms

e Unit 3 MSIV X-room

  • Unit 3 Steam Air Ejector room "A"
  • Unit 2 and 3 Reactor Building (portions)
  • Unit 2 and 3 torus area (El 512 ft.)

b.

Observations and Findings

In general, the observed material condition of most plant equipment was adequate;

however, some areas could substantially benefit from additional licensee attention.

In contrast some areas had received significant attention such as the emergency

service water vaults and adjoining corridors, the Unit 2 heater bay, and the reactor

building equipment drain tank room. Housekeeping was.adequate even.though the

ongoing outages posed a daily challenge.

b. 1

Unit 3 Main Steam Isolation Valve Room

The team identified minor deficiencies such as rust on bolts, piping and pipe flange

connections. There were also some minor structural deficiencies identified such as:

(1) A gland packing nut did meet the minimum thread engagement, and (2) the

team identified a large nut welded to feedwater flued head anchor support that was

not identified on the design drawing. The system engineer initiated Action

Requests (AR) 970037071 and 970037380 to correct the identified deficiencies.

b.2

Steam Jet Air Ejector Room-A

The team observed electrical duct tape wrapped around most piping and valve

flange connections in the Unit 3 steam jet air ejector (SJAE) Room-A. Discussions

with cognizant licensee personnel indicated that the electrical duct tape prevented

in-leakage into the system. The team was informed that this issue was previously

13

identified by the licensee. Work Request 960100762 had been generated to

remove the tape and repair any leaking flanges. The team noted that the material

condition of the nonsafety-related components in the Unit 3 SJAE Room-A was not

adequate to support efficient* plant operations.

The team also identified unapproved rigging attached to a piping system (U3 MS to

3A Relief to Main Condenser) in SJAE Room-A used to lift Valve 3-5406-A-501.

Use of the specific piping as an attachment point for rigging had not been

evaluated. The team found that rigging calculations had been performed on some

piping systems in the room; however, the observed pipe had not been included.

Subsequent calculations performed by the rigging engineer after the team's

observations indicated that the rigging of the valve to the pipe was acceptable.

c.

Conclusions of General Plant Conditions

The team concluded that the general material condition of the plant was adequate

considering a dual unit outage was in progress. Some areas of the plant had

received significant attention in the recent past as part of the licensee's overall

material condition improvement program. Some areas in the "balance-of-plant," or

nonsafety systems, were observed to be in poor condition. Corrective maintenance

documents were initiated, or already existed, to correct the noted deficiencies.

M2.2 Instrument Maintenance Facilities

a.

Inspection Scope (627041

The team inspected the Instrument Maintenance hot shop material condition and

general housekeeping of the facility.

b.

Observations and Findings on Instrument Maintenance Facilities

Housekeeping in the Instrument Maintenance hot shop area appeared to be

adequate. Separation existed between contaminated and non-contaminated tools.

A barrier was erected between contaminated and non-contaminated areas with

survey instruments readily available. The team observed adequate radiological

practices.

c.

Conclusions on Instrument Maintenance Facilities

The maintenance and housekeeping of the Instrument Maintenance hot shop was

adequate .

14

M3

Maintenance Procedures and Documentation

M3. 1 Safety Key Control

a.

Inspection Scope

The team observed an Instrument Maintenance Department (IMO) Control Systems

Technician (CST) perform a surveillance at a test cabinet containing safety-related

instrumentation.

b.

Observations and Findings

c.

On April 14 the team observed performance of Dresden Instrument Surveillance

(DIS) 1600-03, "Torus to Reactor Building Vacuum Relief Valve Trip Unit

Calibrations," Revision 7. The team observed an IMO technician at local analog trip

system (ATS) Panels 2202 (3) -73A and-738, located in the turbine building. Step

D.2 of DIS 1600-03 re*quired the IMO technician to obtain Safety Key CB-1 from

the operation shift supervisor. Step 1.8.a. of DIS 1600-03 required the IMO

technician to "Unlock AND remove trip rack card file locking bar associated with

MTU (Master Trip Unit) AND STU (Slave Trip Unit) ... " A review of the

Operations Department key control log identified that the IMO technician had not

checked out Safety Key CB-1 from the Operations Department; rather, the

technician used an unauthorized key stored in an IMO key locker. At the time of

this inspection, no IMO key control procedures existed.

Dresden Technical Specification 6.8.A required, in part, that written procedures

shall be implemented covering the activities referenced in Appendix A of Regulatory

Guide (RG) 1.33, "Quality Assurance Program Requirements (Operation),"

Revision 2, February 1978. Administrative and maintenance procedures were

referenced in RG 1.33.

Dresden Administrative Procedure (OAP) 7-14, Revision 8, "Control and Criteria For

Locked Equipment and Valves," described the criteria and controls needed for

issuing keys and operating locked valves and equipment.

Procedure OAP 9-13, Revision 6, "Procedural Adherence," described the

expectations regarding the use of and adherence to station procedures.

Contrary to the above, on April 14, 1997, an IMO technician obtained an

unauthorized safety key from an IMO key locker and not from the shift supervisor,

as required by procedure. Failure to properly implement DIS 1600-03, Revision 7,

Step 0.2,is an example of a Violation of Technical Specification 6.8.A

(50-237;249/97007-01 a)

Conclusions

The IMO technician did not follow station procedures to obtain Safety Key CB-1.

The IMO shop had an uncontrolled, unauthorized safety key accessible for general

15

use. The IMO shop did not have a key control procedure for either safety-related or

nonsafety-related keys.

M3.2 Independent Verification

a.

Inspection Scope

b.

The team observed an IMO technician perform a surveillance on the reactor building

ventilation stack flow monitor.

Observations and Findings

On April 18 the team observed the performance of DIS 5700-14, "Reactor Building

Vent Stack Flow Monitor Functional Test," Revision 1. The team observed two

contract IMO personnel performing the test. Step 1.8.c required an independent

verifier to "witness" the lifting of an electrical lead from a terminal block. The team

requested records to verify that the contract personnel were trained to perform

independent verification. The IMO superintendent responded that independent

verification training for the twelve IMO contract personnel had been performed

verbally in the shop and that no records existed to document the training. In

contrast, the station provided information that showed twenty Electrical

Maintenance Department (EMO) contract personnel received formal, documented

training regarding independent verification. A review of OAP. 07-27, "lndepenpent

Verification," Revision 13, identified a difference between the station's *

administrative procedure requirements for independent verification, and what was

implemented in the Instrument Maintenance Department procedures. The concept

of "witnessing" an event was not defined in either the departmental or station

procedures. Conversations with station management identified that IMO procedural

requirements to "witness" were actually a "second check" as defined in the

station's administrative procedures. Specifically, OAP 07-27, "Independent

Verifications," Step F. 1, required that independent verifications be performed on all

lifted leads involving Technical Specification or safety-related equipment. In

addition, the team noted that an "apart in time" independent verification was not

performed as defined by station procedure OAP 07-27.

Dresden Technical Specification 6.8.A required, in part, that written procedures

shall be implemented covering the activities referenced in Appendix A of Regulatory

Guide (RG) 1.33, "Quality Assurance Program Requirements (Operation),"

Revision 2, February 1978. Administrative and maintenance procedures were

referenced in RG 1.33.

Dresden Administrative Procedure (OAP) 07-27, "Independent Verifications,"

Revision 13, Section F.1, required that independent verification be performed on all

lifted leads involving Technical Specification or safety-related equipment.

Contrary to the above, on April 18, 1997, a "second check" was performed in

accordance with DIS 5700-14, "Reactor Building Vent Stack Flow Monitor

Functional Test," Revision 1, Step 1.8.c. That surveillance instruction required an

16

..

independent verifier to "witness" the lifting of a safety-related electrical lead from a

terminal block versus the independent verification required 'by OAP 07-27. Failure

to properly implement OAP 07-27 is an example of a Violation of Technical

Specification 6.8.A (50-237;249/97007-01 b).

c.

Conclusions

A "second check," not an "independent verification" was performed duri.ng DIS

5 700-14. IMO and station administrative procedures were not in agreement

regarding the requirements for independent verification. The training of contractors

on the requirements for independent verification was inconsistent.

M4

Maintenance Staff Knowledge and Performance

M4. 1 Instrument Maintenance Performance

a.

Inspection Scope (62704)

The team observed 24 field maintenance activities performed in the Instrument and

Controls areas. Team observations included various maintenance activities such as

remounting of components, calibration of pressure switches, Technical

Specification surveillances, functional tests of level switches, a vent stack flow

monitor functional test, trouble-shooting and repair of the Unit 2 drywall continuous

air monitor (CAM), post-LO CA containment hydrogen and oxygen analyzer

calibration, turbine trip functional tests, calibration of a resistance temperature

detector, source range monitor rod block calibration, reactor feedwater loop

temperature calibration, and local power range monitor (LPRM) pre-installation

insulation resistance and breakdown voltage acceptance checks.

The team observed all or part of the following work request (WR), dresden

instrument surveillance (DIS) or Dresden instrument procedure (DIP) activities:

DIS 1600-03

Torus to Reactor Building Vacuum Relief Valves Trip Unit

Calibration

WR 940097988-08 Replace Tripping Function Yarway Reactor Water Valve Switch

DIS 2400-02

DIS 5700-04

DIS 0263-07

Post-LOCA Containment Hydrogen and Oxygen Analyzer 18

Month Calibration and Maintenance Inspection

Reactor Building Vent Stack Flow Monitor Functional Test

A TWS RPT /ARI [recirc pump trip/alternate rod insertion] and

ECCS Level Transmitters Channel Calibration Test and EQ

Maintenance Inspection

WR 950060521-01 3A LPCI PMP MOTOR SURVEILLANCE

17

_,

DIS 0250-01

Main Steam Line High Flow Isolation Switch Calibration

WR 960087265-01 Correct Switch Vertical Mounting Position and Calibration

DIS 9900-01

DIS 0700-10

DIS 5600-05

DIS 2300-08

Computer Controlled Analysis Input Instrument Calibration

Source Range Monitor (SRM) Rod Block Calibration

Turbine Trips Functional Test

Units 2/3 Contaminated Condensate Storage Tank and Unit 2

Torus Level Switches Functional Test

WR 950062900-02 Send Out for Refurbishment and Calibrate

WR 970001564-01 2A Off Gas Condenser Normal Level Control

DIS 0202-04

Recirculation Pump MG Set Scoop Tube Control Rod Actuator

Assembly Upper Mechanical and Electrical Stop

WR 960096144-01 Clamp MG Set Scoop Tube and Perform DIS 0202-04

WR 970043047-01 Troubleshoot and Repair Unit 2 OW [drywall] CAM Pegged

Low

DIS 1700-17

DIS 1400-04

DIS 0287-01

NMC Drywall Continuous Air Monitor Preventive Maintenance

and Calibration

Emergency Core Cooling System Fill System Alarm Pressure

Switches

Automatic Depressurization System CS and LPCI Pumps

Discharge Pressure - High (Permissive). Channel Calibration and

Chann~I .Functional Test

WR 970005193-01 River Temp Recorder Calibration

DIS 1600-04

DIP 0700-06

DIS 1600-10

ECCS Drywall Pressure Switches Channel Calibration and

Channel Functional Test

LPRM Pre-Installation Insulation Resistance and Breakdown

. Voltage Acceptance Checks

Drywell and Torus Pressure Instrumentation Channel

Calibration and EO Surveillance for Age Related Degradation

18

b.1

Observations and Findings regarding Instrument Maintenance Technicians

Adherence to Procedures

The team observed two instances where IMO technicians did not follow approved

procedures during the conduct of maintenance:

During performance of DIS 1600-03, "Torus to Reactor Building Vacuum

Relief Valves Trip Unit Calibration," Revision 07, the surveillance performer

did not turn off the power supply to the test modules as directed by the

procedure to secure the equipment in a safe state. (The team identified the

condition to the cognizant supervisor.) The technical concern was if the

equipment remained energized, then a false trip might occur when the

equipment was returned to service.

During performance of DIP 0700:-06, "LPRM Pre-Installation Insulation.

Resistance and Breakdown Voltage Acceptance Checks," the surveillance

performer used Revision 2 of DIP 0700-06; however, that procedure had

been revised and the current "Revision 3" version should have been utilized.

OAP 09-13, "Procedural Adherence," Revision 06, required the user to verify

that the procedure was the current revision or a temporary change. The

licensee generated a problem identification form (PIF) to document that the

maintenance activity was not performed with the current revision and to

document the corrective actions.

Dresden Technical Specification 6.8.A required, in part, that written procedures

shall be implemented covering the activities referenced in Appendix A of Regulatory

Guide (RG) 1.33, "Quality Assurance* Program Requirements (Operation),"

Revision 2, February 1978. Administrative and maintenance procedures were

referenced in RG 1.33.

Failure to turn off the power supply to a test module during performance of

DIS 1600-03; "Torus to Reactor Building Vacuum Relief Valves Trip Unit

Calibration," Revision 07, and failure to verify the proper revision level of DIP

0700-06, "LPRM Pre-Installation Insulation Resistance and Breakdown Voltage

Acceptance Checks," during performance of surveillance testing are examples of a

of a Violation of Technical Specification 6.8.A (50-247/249-97007-02a&b).

c. 1

Conclusions on Instrument Maintenance Adherence to Procedures

With the exception of the instances noted above, the IMD staff was generally

following procedures. The team observed that the IMD had the resources and

capability to improve procedural adherence.

b.2

Observations and Findings on Instrument Maintenance Surveillance Performance

During performance of Unit 2 DIS 0202-04, Revision 01, "Setting Recirculation

Pump MG Set Scoop Tube Control Rod Actuator Assembly Upper Mechanical and

Electrical Stop," Step 1.11.j.3 through 7, the indicated switch contact states were

19

reversed in the procedural steps. The closed state was indicated as open, and the

open contact state was indicated as closed. After consultation with the IMO

supervisor, the technician proceeded with the maintenance with the supervisor's

approval.

During the performance of Unit 2 DIS 1600-04, Revision 14, "ECCS [emergency

core cooling system] Drywall Pressure Switches Channel Calibration and Channel

Functional Test," on page 72 of 81, the procedure erroneously referred to PS

3-1632-B, when it should have been PS 2-1632-B. After consultation with the IMO

supervisor, the technician continued the surveillance with the supervisor's approval.

The table on the page 72 was appropriately marked as not-applicable.

During the performance of Unit 3 DIS 5600-05, Revision 10, "Turbine Trips

Functional Test (Not Tested in Another Procedure)," the technician found that the

temperature switches were out-of-calibration. The technician appropriately

generated two PIFs to identify the out-of-calibration.

During the performance of Unit 3 reactor low level ECCS initiation, Work Request

940097988-08, the technician found that the work task did not specify the correct

machine screw size. The technician appropriately generated an engineering change

notice to identify the correct size screw.

c.2

Conclusions on Instrument Maintenance Surveillance Performance

The IMO maintenance and surveillance activities observed were adequately

performed. When problems were encountered by IMO technicians, supervisors

were there to render assistance to the technicians to complete the jobs.

b.3

Observations and Findings on Instrument Maintenance Preparation

The team observed pre-job briefings for IMO maintenance activities and the

coordination with the Operations Department on specific maintenance tasks. The

team also observed the pre-job walkdown of the job, review of the work package,

. review of the radiological conditions for the job location; and verification of the

revision of the procedures used.

The pre-job briefings were performed per OAP 15-06, Revision 17. The supervisors

conducted a step-by-step briefing of the procedures for the crews performing the

maintenance tasks. The supervisors reviewed the out-of-service requirements of

the job with the crews. The team noted that, for the activities observed, the pre~

job briefings were well conducted.

c.3

Conclusions on Instrument Maintenance Preparation

The team concluded that the job preparation for the activities observed were

appropriate .

20

M4.2 Mechanical Maintenance Performance

a.

Inspection Scope (62703>

The team observed all or portions of the following 23 Mechanical Maintenance

Department work activities:

WR 960100729-01

WR 950065976-01

. WR 960049153-01

WR 940096369-01

WR 950093031-03

WR 960099129-01

WR 960034237-01

WR 950064442-12

WR 950064442-11

WR 950063630-01

WR 950046326-01

WR 950064530-01/02

WR 950061535-01

WR 950061535-02

WR 950061535-03

WR 950061535-04

Trouble shoot and Repair Standby Liquid Control Pump

3-11028

Replace HPCI Turbine Flexible Oil Lines in Oil Reservoir

Repair Stem for Feedwater Heater Normal Level Control

Valve

Replace Extraction Steam Nozzles for Feedwater Heater

Determ and Reterm Limitorque and Limit Switches and

Perform Signature Trace

Disassemble Outboard Turbine Bearing for Unit 3 HPCI

Turbine

Unit 3 HPCI Drain Pot Line Replacement

Replace Valve Trim and Actuator for 3-0642-B

Modification, Replace 3-0642 Valve Trim Assembly

Disassemble Low Flow Feedwater Regulator Valve

(3-0643), Inspect/Repair Valve Seat

Disassemble/Reassemble MSIV for Installing New Liner

Design

Replace Air Diaphragm on Scram Valve 34-31

Replace Accumulator Scram.:Water Cylinders with

Stainless Steel Accumulator

Repair Body to Bonnet Leak and Inspect Valve HCU 42-

31 Cooling Water Inlet Valve

Replace Air Diaphragm on Scram Valves 42-31 Inlet

Valves

Replace Air Diaphragm on Scram Valves 42-31 Outlet

Valves

21

*

b.

b.1

WR 890062254-02

WR 960118148-02

WR 960118198-03

WR 970044365-01

WR 950107745-02

WR 950107745-01

WR 940097084-03

Install Gas Saver Lance on Pipe to Condensate Booster

  • Pump "3B"

Repair Existing Monel Stub Plate for 3B

LPCl/Containment Cooling Heat Exchanger

Repair Existing Monel Stub Plate for 3A

LPCl/Containment Cooling Heat Exchanger

Reinforce Flued Head Anchor Support for Penetration X-

116B

Repair Steam Leak thru the Seat of 3A Off Gas

Preheater PCV 3-5424-A Bypass Valve

Repair Steam Leak thru the Seat of 3A Off Gas

Preheater PCV 3-3099-46 Outlet SV

Repair of Guide Rails for Unit 3 LPCI II Full Flow Bypass

Test Inboard MOV No. 01208

Observations and Findings on Mechanical Maintenance Performance

In general, the team found work performed under the above activities to be

conducted in a professional and thorough manner. Maintenance personnel observed

were experienced and knowledgeable of the assigned tasks. The team frequently

observed supervisory and system engineering oversight of the job activities.

Quality control personnel were also present when required by the work package

and procedure. When applicable, appropriate radiation control measures were

established or in place.

Observations and Findings on Reactor Feedwater Regulating Valves

The team observed work activities for the Unit 3 reactor feedwater regulating

valves. The work being performed was a modification initiated by the licensee as

corrective actions implemented to improve the reliability of the feedwater system.

The team noted that the licensee was in the process of purchasing a software

package "Valve Packing Optimization Program (VPOP). This software could reduce

manhours, and eliminate the possibility of incorrectly selecting the proper size

packing for any particular size valve at the Dresden site. This program could also

eliminate extra burden from work analyst. The team noted the use of VPOP was an

excellent tool for valve maintenance.

The team observed various portions of work being performed on the reactor

feedwater regulating valves. The team observed maintenance technicians install an

actuator on Valve 3A, and take measurements for the installation of Valve 3B

internals. The work being conducted was a modification to improve feedwater

22

b.2

regulating valve reliability which was also a long term corrective action fix. The

work was being conducted by a contracted valve maintenance group. For the

activities observed, workers were knowledgeable of the work being conducted, and

work was performed in accordance with procedures. Supervisory oversight was

good.

Observation and Findings on Main Steam Isolation Valve Repair

The team observed repairs to Main Steam Isolation Valve (MSIV) 3-0203-28. The

team observed removal of the internals from the valve and noted that the

radiological controls were good during breach of the system. The team* observed

good supervisory oversight. Maintenance technicians were knowledgeable and

experienced.

In addition, during the above activity observation, the team noted the following:

Poor radiological practices by a maintenance worker (carpenter) in the MSIV

X-room was observed by the team. The maintenance worker did not have

the appropriate minimum protective clothing (scrubs) as required by OAP

12-35, *oonning And Removal Of Routinely Required Radiological Protective

Clothing And Protective Clothing Guidelines," Revision 4. The team

questioned th.e maintenance worker about the proper protective clothing.

The maintenance worker wore blue jeans instead of scrubs while placing

tags on a scaffold. Procedure OAP 12-35 required minimal protective

clothing to be worn when conducting work activities, and the team believed

that crawling over pipe to hang tags on scaffold was work. Discussions

with various radiation protection technicians indicated inconsistericies in how

the procedure was being implemented. It was also not clear what

management expectations were with regards to the minimum protective

clothing requirements. The team informed licensee management of this

issue.

During observation of maintenance activities in the MSIV X-room, the team

observed the following:

On April 17, 1997, foreign material exclusion (FME) controls were not

adequate in the MSIV X-area as evidenced by protective clothing, rubber

shoe covers, plastic protective clothing, rags and rubber gloves laying in

disarray throughout the area.

On April 17, 1997, electrical maintenance personnel were observed not to

replace a valve cover for MOV 3-220-3 for about 2 1 /2 hours after leaving

the area, which left the limit switches and electrical connections

unprotected.

Dresden Technical Specification 6.8.A required, in pa.rt, that written procedures

shall be implemented covering the activities referenced in Appendix A of Regulatory

Guide (BG) 1.33, "Quality Assurance Program Requirements (Operation),"

23

b.3

  • -

Revision 2, February 1978. Administrative and maintenance procedures were

referenced in RG 1.33 .

Dresden Administrative Procedure (OAP) 03-23, "Foreign Material Exclusion

Program," Revision 8, required in part: O) FME controls are required for any work

activity, modification, test, inspection or sampling that involved opening a system

or component; (2) extra protective clothing, equipment, tools and parts not

immediately used that are brought into an FME area will be properly contained while

no work was in progress, and (3) Covers must be placed on all systems breached

when the opening was left unattended.

room on April 17, 1997, as discussed in the two instances above is an example of

a Violation of Technical Specification 6.8.A (50-237;249/97007-03a&b).

The team also identified several valves that did not appear to be in accordance with

the HPCI system valve checklist or the inaccessible locked valve checklist. The

HPCI system checklist indicated that Valve 3-2399-87 and 3-2301-97C should

have been closed and locked. Actual field configuration indicated that Valve

3-2399-87 was not locked. The revised inaccessible locked valve checklist deleted

these valves from being locked; however, Valve 3-2301-97C was closed and

locked in the field configuration. The team discussed this issue with the cognizant

licensee engineer, and discussions indicated that the noted problem had been

identified previously and corrective action was in the progress of being

implemented. The team was informed that the inaccessible locked valve checklist

had been revised as part of the completed corrective action. Further, the team was

informed that all corrective actions were required to be completed prior to the

completion of the current outage (03R14). The team noted however, that no plan

had been implemented at the time of the inspection to complete the proposed

corrective actions. Corrective action began in March 1995 and were sched.uled to

be complete this outage (03R14).

Observations and Findings on Control Rod Drive Scram Discharge Valve Repair

The team observed General Electric technicians remove old air diaphragms and

install new diaphragms in Scram Discharge Valves 126 and 127. The team

questioned the technicians on various portions of the work package and

instructions. The technicians were knowledgeable and professional, and there was_

good supervisory oversight of the work activities.

During a plant tour, the team observed old and new control rod drive scram

solenoid pilot valves in an unspecified FME Zone area in Unit 2. The new valves

were to be installed in Unit 3. The new valves were not fully protected at the pipe

ends to prevent dirt and debris from entering and degrading the valves. Failure to

follow the foreign material exclusion (FME) requirements of OAP 03-23 for the CRD

scram solenoid pilot valv~s is another example of a Violation of Technical

Specification 6.8.A (50-237;249/97007-03c).

24

b.4

b.5

Observations and Findings on Condensate Booster Pump Piping Repair

The team observed maintenance technicians perform a hydrostatic test on the gas

saver lance on pipeline B. The technicians followed procedures; however, the

technicians indicated that during a previous hydrostatic test, the post calibration of

the pressure gage indicated the gage was well out of tolerance. The team

questioned whether a PIF was written because the gage could have been used on

safety-related equipment. The PIF was not written by the individual technicians

until prompted by the team, which indicated some reluctance or lack of knowledge

of the involved technicians on when to initiate a PIF.

Observations and Findings on Low Pressure Coolant Injection/Containment Cooling

Heat Exchanger Repair

The team observed maintenance personnel perform welding activities on Unit 3 low

pressure coolant injection (LPCI) and/or containment cooling heat exchanger "A"

and "B." Maintenance technicians were repairing the divider plate in both heat

exchangers due to degradation. The team observed welding of the monel stub

plate on both heat exchangers. On April 22 the team identified two instances

where procedural requirements were not fully adhered to:

During welding of FW 1 and FW 2 for "38" heat exchanger, the welder did

not verify interpass temperature as required by the weld data sheet and

Weld Procedure NSWP-W-01, "ASME and ASME 831 . 1 Welding,"

Revision 3. Discussions with maintenance engineering personnel performing

the work indicated that interpass temperature was verified based on welder

experience. The weld data sheet to the work package specified a maximum

interpass temperature of 700°F. The maintenance technicians at the work

location did not verify the interpass temperature. Also, the technicians did

not have a temperature stick or pyrometer at the work location to verify

interpass temperature.

Through discussions with the cognizant welding engineer, the team learned

that the expectation for how to determine interpass temperature was at the

discretion of the welder. Upon completion of this discussion, the cognizant

welding engineer initiated a memorandum dated April 23 to all Dresden

welders indicating when interpass temperature was specified, interpass

temperature must be verified upon completion of a weld pass.

Dresden Technical Specification 6.8.A required, in part, that written procedures

shall be implemented covering the activities referenced in Appendix A of Regulatory

Guide (RG) 1.33, "Quality Assurance Program Requirements (Operation),"

Revision 2, February 1978. Maintenance procedures were referenced in RG 1.33.

Failure to verify interpass temperature as required by the weld data sheet and Weld

Procedure NSWP-W-01, is an example of a Violation of Technical Specification 6.8.A (50-237;249/9707-04a).

25

-,

b.6

During the second shift, maintenance technicians were observed performing

welding activities on the "38" heat exchanger monel stud plate without the

proper work package. The work package had been retrieved from the area

  • for revision by the work analyst; however, a minimal work document was

left for the maintenance personnel to continue work. Procedure OAP 15-06,

"Preparation, Approval, and Control Of Work Packages and Work Requests,"

Revision 17, required at a minimum, a copy of the work request for portions

of work being performed that day. The minimal work document was not

sufficient for the work activities being performed on the heat exchanger 38

monel stud plate. The maintenance superintendent immediately stopped

work and initiated a PIF.

Failure to have the appropriate work document as required by OAP 1 5-06 is another

example of a Violation of Technical Specification 6.8.A (50-237;249/97007-04b).

Observations and Findings on Unit 2 Flued Head Anchor Support

The team observed welding activities performed. on Unit 2 flued head anchor

support 2-1600-X-1168. The licensee had identified that several welds on this

containment penetration anchor frame were outside FSAR stress limits. Therefore,

Design Change E12-2-97-206 was implemented to reinforce the welds on the

support. The team found that maintenance personnel did an. excellent job in

surveying the proposed work activities prior to performing any welds. Welders

were qualified to perform the welds made in accordance with the welder

qualification matrix. Overall, the maintenance technicians did a good job.

However, the team noted that Design Change Drawing 8-2088, Revision A, was

very difficult to understand.

The team also noted through subsequent discussions with the cognizant welding

engineer that the licensee had identified that incorrect preheat was specified in the

work instructions by the work analyst. Preheat should have been 1 50°F instead of

the noted 50°F. For this task, the team observed that: ( 1) work analyst may have

been tasked with responsibilities that engineering could more appropriately p_erform,

such as specifying preheat requirements, and (2) expediting emergent work

activities without adequate review appeared to have resulted in some poor work

documents.

b. 7

Observations and Findings on Unit 3 Off Gas Preheater Pressure Control Valve

Replacement

The team observed maintenance technicians perform Weld 5 and Weld 1 on the 3A

Off Gas system Pressure Control Valves 3-3099-46 and 3-3099-48 and associated

pipe attachments. Fitup was performed properly, and the welders were

knowledgeable of the work requirements and the procedure used. The team also

verified the welders were qualified in accordance with the welder qualification

matrix. The work activity was conducted in an excellent manner.

26

b.8

c.

Observations and Findings on Unit 3 LPCI Valve Repair

The team observed maintenance technicians install valve internals to Motor

Operated Valve (MOV) 01208. This valve was apparently having problems with the

guide rails .. Maintenance technicians performed an excellent job installing the valve

internals. Procedures and instructions were followed *. The team found that the

maintenance technicians performing the work were both ComEd and contractor

technicians. For the work observed, the assigned craft worked well together. The

team also observed quality control perform FME verification. Discussions with the

technicians indicated that quality control had written a PIF on the valve disk

because of deficiencies identified during a dye penetrant exam. The team was

informed by the licensee that engineering conducted an evaluation, and determined

the disk to be acceptable.

General Conclusions on Mechanical Maintenance Performance

Mechanical Maintenance activities were generally conducted in a thorough and

professional manner. The team identffied two specific violations with multiple

examples of each. The violations involved poor FME controls; inadequate welding

processes; and performance of safety-related work without a sufficient work

package at the work site. In addition, some poor work practices were identified

with regard to minimum protective clothing requirements and unanalized rigging of

components to nonsafety piping systems.

M4.3 Electrical Maintenance Performance

a.

Inspection Scope (62703)(62705)

The team observed or reviewed all or portions of the following 14. Electrical

Maintenance Department work activities:

WR 970042480-01

WR 970042481-01

WR 950018438-01

WR 960027460-01

WR 960066023-01

WR 970020861-01 *

WR 950068428

Addition of Restraining Straps on GGS 4 KV Circuit

Breakers Using Design Change (DCN) 001086E

Addition of Restraining Straps on GGS 4 KV Circuit

Breakers Using DCN 001086E

250V DC Station Battery Cell Maintenance Unit 3

Unit 3 250V Station Battery Modified Performance Test

125 V Molded Circuit Breaker Inspections and Testing

Using Procedure SMP-E-01

Seal Various Penetrations in Technical Support Center

HVAC

Unit 3 Six Year Exciter and Generator Inspections

27

,..

WR 960098283-01

WR 960097439-01

WR 960110681-01

WR 950060779-02

WR 950060659-01

WR 970046098-01

Temp Alt 11-07-97

Replace Limit Switches on 1 A and 1 C Main Steam

Isolation Valves and Perform Surveillance Check

Afterwards

Inspect Ground Device # 10 and Shim if Required

Repair Motor Oil Leaks to the 2A Reactor Recirculation

Pump

Perform Preventive Maintenance and Inspect the Unit 3,

"B* Channel, Reactor Protection SCRAM Contacts

Perform Preventive Maintenance on the Contactor to a

DC Motor for the HPCI Condensate Storage Tank

Return Valve

Troubleshoot and Repair a Full Negative Ground in the

Unit 3 125 V DC System

345 KV Bus 6 Bypass for New Line 2311

b. 1

Observations and Findings on Switchyard Work on 345 KV Lines (All Units)

The licensee initiated a modification to install a 345 KV tie line between the

Dresden and Collins (fossil plant) station switchyards. To support work on the

modification, the licensee prepared a temporary wood pole structure to bypass

345 KV Bus 6 and keep the Dresden station blue bus ring intact. The team

observed work in the switchyard, reviewed associated documentation, and

discussed the job with licensee personnel.

While watching modification activities in the field, the team observed that the

licensee had installed a temporary security fence (within the main switchyard

boundaries) to direct vehicle and heavy equipment traffic away from vulnerable

switchyard structures. Discussions with the licensee personnel revealed that, prior

to the teams' arrival on site, the crew performing the task was required to perform

five practice setups and removals of the 85-foot long wooden poles prior to

commencing actual work in the switchyard. The team observed portions of the

actual switchyard work and identified no concerns. Through discussions with

cognizant licensee personnel and review of the associated documentation, the team

noted that the plant onsite review committee (PORC) had twice rejected the

modification package plans prior to recommending approval of the project.

c. 1

Conclusions on Switchyard Work on 345 KV Lines (All Units)

The team concluded that the work performed in the switchyard was appropriately

controlled and conducted in a manner to minimize the possibility of an offsite power

28

interruption. The team considered the PORC's rejection of the initial package to be

a positive indication of a strong and independent review process.

b.2

Observations and Findings on Modifications to 4KV Circuit Breakers Auxiliary

Switches <Unit 2 and 3)

On April 10, 1997, the licensee shut down Unit 2 after declaring some Merlin-Garin

4KV circuit breakers inoperable. Licensee personnel had discovered cracks in the

offsite power supply breaker to the diesel emergency bus and declared all offsite

power supply busses inoperable. The team observed in-plant temporary repairs to

the breakers and reviewed the associated documentation.

The team observed in-plant repair activities to address cracks that were discovered

in some of the auxiliary switches of the 4KV Merlin-Garin breakers. The team

observed electrical maintenance, quality control, and engineering personnel at the

job site; all appeared knowledgeable of the issue, and the team observed effective

communication and coordination between the groups when the work activities took

place. However, the work was suspended on the breakers due to licensee

identified concerns with the work instructions. Discrepancies were noted between

engineering documents and work package instructions in the field. Specifically, not

all PORC comments were incorporated into the work package and inconsistencies

existed in the inspection criteria used to accept the work. The licensee initiated a

problem identification form (PIF) to document the work package deficiencies. The

work package instructions were subsequently clarified and the team identified no

further concerns with the work.

c.2

Conclusions on Modifications to 4KV Circuit Breakers

The team concluded that personnel in the field worked effectively to install the

breaker repair modification and that licensee personnel appropriately halted work

when discrepancies were noted in the work package instructions. However, the

team also concluded that the initial work package was poorly planned.

b.3

Observations and Findings on Unit 3 Station 250 VDe Battery Modified

Performance Discharge Test

The licensee conducted a modified performance test (MPT) of the Unit 3 250 voe.

battery. The test was intended to satisfy the requirements of both a service test

and a performance test. The team observed portions of the MPT, reviewed the

procedures, and followed up on questions developed during the reviews.

The team observed test preparations and portions of the testing activities. The

performance of the test was delayed because the required test equipment was not

initially available to support testing. The delay was due to the failure to have

appropriate cable connectors for the load banks available onsite when the licensee

initially was scheduled to conduct the modified performance test.

29

Test performance and results:

At the start of the inspection, the team developed concerns regarding the licensee's

testing methodology of the Unit 3 250 voe battery. The concerns centered around

the testing of the battery in the .. as found* condition. The licensee performed a

MPT as allowed by Technical Specifications (TS); however, the TS stated that the

modified performance discharge test satisfied the requirements of both a service

test and the performance test [defined in IEEE 450-1995).

Prior to testing the battery using the service test methodology I the licensee was

restricted from testing the battery in any condition other than the *as found"

condition. The MPT was required to meet the initial conditions of the service test,

and performance of maintenance prior to the test would invalidate the "as found"

condition of the battery.

Substantial maintenance was performed* on the station battery prior to the MPT.

The maintenance included:

o

Replacement of cell Number 48

Replacement of inter-tier cables

Replacement of a large number of battery post seals

Cleaning of the battery connection posts

The team's review of battery data showed that replacement of cell Number 48 was

due to the identification of a small crack in the battery housing and not due to a

low voltage of the cell. In addition, cleaning of the battery posts improved the

inter-cell resistance values, but only by about 20 percent. The team, assisted by *a

Region Ill specialist inspector, concluded that the above maintenance pre-

conditioning of the station battery did not make a significant difference to the

results of the test; however, pre-conditioning did occur.

The licensee's performance of the pre-test maintenance was contrary to the TS

requirement to perform the MPT in the "as foundR condition, i.e., a MPT was

intended to meet the requirements of a service test. Initially, cognizant licensee

personnel believed that performance of the pre-test maintenance activities did not

make a significant difference in the battery's ability to perform its function;

therefore, the licensee believed the pre-test maintenance did not violate the "as

foundR requirement.

In addition to the pre-test maintenance, the Unit 3 250 VOC battery was given a

222-hour equalize charge starting on April 3, 1997, in anticipation of the scheduled

MPT. The equalize charge on the battery just prior to the test discharge was

performed in accordance with Work Request 950018438-04, "Perform Equalize

Charge." The equalize charge work request was apparently initiated to satisfy

Dresden Electrical Surveillance (DES) 8300-20, "Unit 3 250 Volt Station Battery

30

Modified Performance Test," Revision 02, Step G.3, which stated: "Equalize

charge is recommended within 30 days prior to the test, but

NOT within three

days prior to this test."

Step G.3 of DES 8300-20 was essentially a verbatim translation of the Institute of

Electronic and Electrical Engineers (IEEE) 450-1995, Section 6.1 "Initial

Conditions," Requirement a), which stated .. Equalize the battery if recommended by

the manufacturer and then return it to float for a minimum of 72 h, but less than

30 days, prior to the test." Further, Requirement b) of IEEE 450-1995,

Section 6.1, stated to "Check all battery connections and ensure that all resistance

readings are correct for the system."

However, IEEE 450-1995, Section 6.6, "Service Test," stated, in part, "The initial

conditions shall be as identified in 6. 1 [omit requirement a), perform requirement b)

but take no corrective action unless there is a possibility of permanent damage to

the battery and perform requirements c) through f))." Therefore, DES 8300-20,

Revision 02, Step G.3, was in error and should have cautioned the test performers

nQ1 to perform an equalize charge. The error in DES 8300-20 was apparently made

when the MPT procedure was originally written in response to the licensee's

endorsement of the 1995 IEEE standard, and a similar step in the old "performance

test" procedure was carried over to the MPT procedure.

Technical Specification 4.9.C.5 stated, in part, that at least once per 60 months,

verify that the battery capacity is at least 80 percent of the manufacturer's rating

  • when subjected to either a performance test or a modified performance test

discharge. The modified performance discharge test satisfies both the service test

and performance test and therefore, may be performed in lieu of a service test.

Since the MPT was subject to the same criteria as a service test, the test was

required to be performed in the "as-found" condition as discussed in the Technical

Specification Bases 3/4.9.C. Failure to perform a MPT in the "as found" condition

is a Violation of Technical Specification 4.9.C.5 (50-237;249/97007-05).

The team reviewed, with the assistance of a Region Ill specialist inspector, the

licensee's operability determination (Document ID 97-69) initiated on May 3, 1997,

to document the licensee's technical evaluation of the Unit 3, 250 VDC battery

with regard to the as-left condition following the MPT. The team concluded that

the Unit 3, 250 voe battery was operable based on the minimum effect the actual

pre-test maintenance had on the battery's performance, as demonstrated and

measured during the actual test. In addition, the team concluded the equalizing

charge, by chance, did not elevate the battery voltage above what would be an

acceptable float voltage prior to test performance. Subsequent to the inspection,

Dresden Licensee Event Report 97-005, dated May 16, 1997, was submitted to the

NRC, which documented the licensee's evaluation and corrective action for the

failure to properly perform the MPT.

On April 10, 1997, a scheduled pre-maintenance work package review identified

that DES 8300-20, Step E.3, required the MPT to be conducted in the "as found"

condition. The system engineer (test director and cognizant supervisor for the

31

MPT) was contacted and informed that the planned maintenance activities could

prevent meeting the "as found" prerequisite of DES 8300-20, Step E.3. Believing

the "as found" condition was not a "requirement," the system engineer contacted

corporate engineering for an assessment of the "as found" requirement. Corporate

engineering memorandum DOC No. DG-97-000513, dated April 14, 1997,

recommended that the "as found" requirement be waived. On April 17, 1997, the

system engineer (test director) attached the corporate memorandum to the test

procedure and noted on Attachment G that: "Battery is not being tested in the "as

found" condition as required in prerequisite E.3."

The system engineer, with the concurrence of corporate engineering, revised the

procedure to delete the as found requirement. That procedural revision was made

outside the Dresden station procedural controls and/or processes.

Dresden Station Technical Specification 6.8.A required that written procedures shall

be established, implemented, and maintained covering the applicable procedures

recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.

Appendix A of Regulatory Guide 1.33,* Revision 2, February 1978, referenced

administrative procedures, procedure adherence and temporary change method, and

procedural review and approval.

Dresden Administrative Procedure (OAP) 09-13, "Procedure Adherence,"

Revision 6, Step F.9.a & .c required the cognizant supervisor to ensure: a) "If the

Procedural Intent will be affected, THEN perform step F.2.a of this procedure," and

c) "Applicable prerequisites are met." Step F:2.a required that the cognizant *

supervisor terminate use of the procedure OR perform a permanent change in

accordance with station procedure and revision processing.

On April 17, 1997, the cognizant supervisor (test director) changed DES 8300-20,

based on a corporate engineering recommendation that the "as found" requirement

be waived. Deleting the "as found" prerequisite was a*n intent change. Failure of

the cognizant supervisor to terminate use of DES 8300-20 OR to perform a

permanent change in accordance with station procedure and revision processing is

a Violation (50-237;249/97007-06).

c.3

Conclusions Unit 3 250 VDC Battery Modified Performance Discharge Test

The licensee's performance of the Unit 3 modified performance discharge test on

the 250 V battery was inadequate in that it failed to comply with plant Technical

Specifications concerning the requirement to be tested in the uas found" condition.

In addition, changes. were made to the battery test procedure which did not receive

the required review by station administrative procedures.

b.4

Observations and Findings on Molded Ca_se Breaker Maintenance

While observing breaker work in the electrical shop, the team discussed the planned

work with electrical maintenance personnel. At the time of the observation, the

maintenance personnel had stopped work on the task and contacted engineering

32

personnel for assistance in correcting an inadequate work package. The work

instructions directed electrical maintenance to reference a separate document to

inspect and test the breaker. The referenced procedure was not correct for the

specific breaker and did not provide correct inspection and testing criteria. The

team observed the initial response to the work instruction error. The maintenance

technician stopped work and contacted engineering for assistance, and the licensee

initiated a PIF to document and resolve the problem.

c.4

Conclusions on Molded Case Breaker Maintenance

The team concluded that maintenance personnel responded appropriately to the

procedural deficiency. However, the incorrect work package instruction

represented an example of poor pre-job preparation.

b.5

Observations and Findings on Troubleshooting of a 125 VDC Ground <Unit 3)

The team performed routine inspection activities of the licensee's followup to a full

negative ground on the Unit 3, 125 VOC system. Portions of the electrical field

work activities were observed and a subsequent review of the work documentation

was also performed.

The electricians involved in the identification of the source of the ground utilized

OAP 15-07, "Electrical/Instrument Maintenance Troubleshooting Procedure (W-1),"

Revision 05. The. team observed electricians in the field attempting to re-land four

wires that had been lifted by a previous work crew. The team observed that the

assigned electricians failed to utilize adequate self check techniques and initially

went to the wrong cabinets in search of the lifted leads. Subsequently, the

licensee initiated a PIF on the inadequate self-check to document immediate and

planned corrective actions.

c.5

Conclusions Troubleshooting of a Ground on the 125 V DC System (Unit 3) *

The team's observations of the troubleshooting of the Unit 3, 125 VOC ground

noted that the assigned electricians initially failed to perform an adequate self-

check.

c.

General Conclusions on Electrical Maintenance Performance

In general, the performance of electrical maintenance activities observed appeared

to be properly planned, performed, and documented. Workers appeared to be

knowledgeable and capable of performing the work activities. The TS battery

surveillance problem appeared to be isolated, but the fundamental problem

regarding procedural controls was significant .

33 '.

MS

Miscellaneous Maintenance Issues

MS.1 Maintenance Backlog

a.

Inspection Scope

The team reviewed the station's backlog of maintenance tasks to evaluate the

licensee's understanding of the cu~rent status. For the purpose of this inspection,

the team utilized the licensee's computerized station backlog data base for action

requests, work requests non-outage, and work requests outage. In addition, a

general review of all maintenance tasks was performed which included a review of

the total station corrective, preventative, modifications, facility, other, and

unknown categories. The computer data base was utilized by the team for

selection of a sample of specific action requests and/or work requests based on

significance, age, and planning status. The review of specific maintenance tasks

was performed by review of station records, interviews of cognizant licensee

personnel (e.g., system engineer), and in some cases through direct field

observations of the maintenance task.

b.

Observations and Findings

b. 1

Action Request Backlog

The Powerblock Backlog for action requests (ARs) dated April 16, 1997, was

utilized for review of the station's AR backlog. That report detailed the current AR

backlog and categorized the 254 open ARs. The AR Powerblock Backlog contained

four categories, which included origination (7), hold awaiting approval (223),

approved (1 ), and minor (23).

The initiating document to perform all work at Dresden was the AR. In general,

only minor maintenance activities in the powerblock could continue to be performed

with only an AR (e.g., change light bulb, paint hand rail, etc.). If more than minor

maintenance was required, a work request was necessary. The AR backlog was

further divided into sub-categories based on outage and non-outage work. The

team reviewed in detail the 220 ARs coded non-outage and on hold awaiting

approval. The team noted that the majority of ARs in the "non-outage on hold

awaiting approval" category (183) had an average age of 11 days. However, a

sub-set of 37 ARs coded as corrective "non-outage on hold awaiting approval" had

an average age of 72 days. Through discussions with c~gnizant station personnel,

the team learned that the corrective ARs coded as non-outage on. hold awaiting

approval were actually approved for work by the station's fix-it-now (FIN) team and

the intent was to capture work when completed, i.e., as the FIN team reported

work complete, the status of the item would be changed to "completed." The

team was able to directly observe the licensee's process through attendance at a

daily action request screening meeting; however, the computer coding for all

ComEd stations showed Dresden was the only ComEd station that was using the

on-hold awaiting approval code to track ARs coded corrective to closure.

34

c.1

The team concluded that the AR backlog was relatively low and only contained

tasks that would not require a station work request to accomplish.

b.2

Work Request Backlog

The Backlog Average Age report dated April 16, 1997, was utilized for a review of

the station's maintenance work request (WR) task backlog. That report detailed the

current WR task backlog and categorized the station's 11,805 maintenance tasks.

The maintenance tasks were categorized into corrective (2743), preventative

(6782), modifications (721), facility (516), other (1042), and unknown (1).

In order to evaluate the validity of the maintenance backlog, the team selected a

representative sample of work request tasks, discuss~d the current status of each

task with cognizant licensee personnel, and in some cases, performed direct field

observations of the deficient condition. Of particular interest were WR tasks

(outage and non-outage) that appeared to be significant, were more than one year

in age, and had not yet been planned.

b.2.1 Non-outage Work Request Tasks

Non-outage WR tasks reviewed included the following:

Task Number

EM

WR 940099081-01

WR 950068772-01

WR 950096403-01

WR 950102600-01

WR 960013596-01

IC

WR 950105270-01

WR 9601168~9-01

WR 960119324-01

WR 970014631-01

WR 970018642-01

MM

WR 940099406-01

WR 950121192-01

WR 960031482-01

WR 960033231-01

WR 960077518-02

Status *

22

22

22

22

22

23

22

22

22

22

22

25

22

22

45

Description

Torus spray electrical breaker trip

Diesel generator control circuit

Inboard MSIV solenoid lights panel

Reactor control panel isolation barrier

Replace Unit 2/3 DG frequency relay

. CRD charging water header gage ruptured

Control room refrigeration pressure gage

Crib house temperature gage broke

Oxygen concentration meter broke

Drywall radiation monitor trip

CRD hanger rod tied off to station

Inlet valve missing flange bolts

CCSW [containment cooling service water] pipe

support spring can adjustment

SBLC [standby liquid control] outboard drain

valve stuck open

Control rod drive water pump

  • Task status codes referenced in the above table were defined as:

35

Status 22 = Investigation not required (task originated);

Status 25 = planning complete; and

Status 45 = task ready.

b.2.2 Non-outage work request task soecific observations:

Work Request Task 940099081-01 was initiated on December 2, 1994, to adjust

breaker trip settings on Low Pressure Coolant Injection (LPCI) Valve 2-1 501-188.

In response to concerns about spurious reverse-current tripping of motor operated

valves, described in Licensee Event Report 50/237-94-030 dated December 23,

1994, a number of motor operated valves were initially identified as potentially

having motor trip settings that were too low. Although initially prioritized as a "81"

(urgent-work start within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />), the task had since been down-graded to a "C"

priority (routine work). Through discussions with cognizant licensee personnel and

review of historical inspection records, the team learned that the LPCI 2-1501-188

valve's motor had sufficient margin to preclude spurious trips and the urgent

classification was no longer required. The as-left breaker trip values for MOV 2-

1501-188, when last tested on October 1, 1990, were adequate to eliminate this

valve from the original suspect population and the current work task was no longer

needed. The team identified that another open work task, not in the team's original

inspection sample (WR Task 94009908201 for Reactor Water Cleanup Valve 2-

1201-1), was similar in that the original task to adjust motor trip settings was no

longer necessary. The team noted that these two work tasks were confusing the

known backlog of non-outage work .

Work Request Task 950096403-01 was initiated on September 30, 1995, to

address a foreign material entry point for an electrical panel for main steam isolation

valve (MSIV) pilot indicating lights. After direct field observation, accompanied by

cognizant licensee personnel, the team observed that the existing condition was not

an immediate concern to the integrity of the electric panel and was properly coded

for routine non-outage work.

Work Request Task 970014631-01 was initiated February 6, 1997, to address a

broken Unit 2 Drywell local oxygen concentration meter. The team identified that

the same meter was the subject of WR 930053045, written in 1993, but that WR

was closed out, without repair, and the licensee was tracking the known deficiency

against open Engineering Request 9503291. The 1997 WR was written since no

immediate information was present in the field to identify that the engineering

request already existed. The licensee annotated the existing 1997 WR to reflect it

would remain open until the engineering request was worked, and a "two-part" tag

was to be hung in the field on the oxygen meter to identify that the deficiency was

a known problem.

Two non-outage WR tasks were identified by the team as being coded incorrectly.

Specifically, WR Task 970037904-01 and 950118049-02 involved work in the

Drywell, but both tasks were coded as non-outage. The Drywell was not normally

accessible during plant operations and the tasks should have been coded to be

performed during an outage .

36

c.2

b.3

Work Request Task 950102600-01 was initiated October 20, 1995, to repair an

isolation barrier for a terminal block inside a reactor control panel. The team

directly observed the deficient condition, and the licensee's classification of non-

outage routine work was considered reasonable.

The team concluded that the non-outage work request backlog contained tasks that

were appropriate to be completed while the units were either operating.

Outage Work Request Tasks

In addition to the non-outage tasks above, the team selected a representative

sample of outage tasks scheduled to work in future refueling outages. The

inspection sample included tasks scheduled for the next Unit 2 or Unit 3 refuel

outage, i.e., D3R15 or D2R15. The non-outage work request tasks reviewed

included the following:

Task Number

Status

.CE/CM/EM

WR 950064036-01

25

thru

WR 950064105-02

EM

WR 950041246-01

22

WR 950066503-01

45

WR 970019996-01

22

GE

WR 950066654-01

45

MM

WR 890063385-01

22

WR 910053212-01

25

WR 930049144-01

25

WR 930053086-01

22

. WR 940098057-01

45

Description

Drywall fan blade adjustment to rated flow

(note: the Drywall work involved 13 separate

work request tasks that were initiated to resolve

concerns with the Drywall ventilation system)

Cracked end bell on HPCI aux oil pump

Replace 3C drywall cooler motor and fan

DC MOV has open shunt field

Hydraulic Control Unit (HCU) leaks

Note: there were a number ( > 100) of small

(single drop) body to bonnet leaks on small

.

manual valves in the HCU system.* The known

Unit 3 leaks were captured on 4 7-work request

tasks.

2A MG set oil cooler outlet valve leak

Adjust oil pressure to main bearing

Turbine building supply fan bearing

Unit 3 HVAC inspection doors

Adjust spring can on

37

b.3. 1 Outage work request task specific observations:

The station's computer listing of all 11,805 station maintenance tasks included one

item that was categorized as *unknown," and at the time of the inspection that

item was 287 days old. The unknown item was identified to be a preventative

maintenance task captured in WR Task 960023216-02. That task was intended to

assure the proper 0-rings were used as replacements during an EO surveillance on a

low pressure coolant injection (LPCI) motor oil sightglass inspection. The unknown

classification was due to a coding error.

Work Request Task 950064036-01 and associated tasks were initiated in July

1995 to adjust fan blades and restore "rated flow* to the Unit 3 Drywall coolers.

These tasks were not being worked during the current Unit 3 refuel outage

(D3R14), but were deferred to the next Unit 3 refuel outage (D3R15). During the

current refuel outage, additional ventilation flow information (e.g., cooler fan motor

amperage and system flow rates) was being obtained to better assess the need for

fan blade adjustments. Through discussions with the system engineer, the team

learned that adequate Drywall flow existed to meet operating parameters, and the

licensee's decision to defer any field work pending the results of further testing was

reasonable.

Work Request Task 950066503-01 initiated in July 1995 was originally intended to

replace Drywall cooler fan motor 3C during the current Unit 3 refuel outage

(D3R14). However, due to a parts availability problem, the task was deferred until

the next refuel outage (D3R15). Through discussions with the system engineer,

the team learned that the subject task was part of a planned system predictive

maintenance effort to replace all Drywell cooler fan motors. The team noted that

during the current refuel outage (D3R 14), Drywall cooler fan motor 3A was being

replaced under WR Task 950066504-01. Since the existing 3C Drywall cooler fan

motor was still performing well, the team concluded the licensee's decision to defer

the subject work to the next refuel outage was reasonable.

Work Request Task 950066654-01 and other associated tasks were initiated

between August 1995 and October 1996 to repair leaks on small manual valves on

the control rod drive system's hydraulic control units (HCUs). As discussed in

licensee electronic memorandum, "Paul Chanell to Frank Spangenberg," dated

April 24, 1997, the decision to defer a number of tasks on small HCU manual

valves was based on a root cause investigation plan that was being implemented by

station engineering. The licensee was in the process of inspecting and replacing

25 of the subject valves in an attempt to identify the root cause for continued

problems with the subject manual valves. Initially, all leaking valves were proposed

to be repaired; however, the licensee deferred a number of valve repairs pending

the root cause determination. The licensee's decision to defer repair on some

valves was based on the criteria that the valve was outside the system hydro

boundary, and a catch basin or funnel was not required to capture the small amount

  • of leakage. .

38

c.3

The team concluded the outage work request tasks were appropriately assigned to

work during a unit outage. In addition, the licensee provided reasonable

explanations for work tasks that deferred to future outages.

b.4

Non-outage Corrective Tasks Backlog Assessment

Over the last several years, the licensee has focused attention on the backlog of

"non-outage work request" as a measure of overall station performance in the area

of corrective maintenance. At the time of this inspection, the non-outage WRs had

been further refined to define the specific number of "tasks" for each WR. This

definition was used at all six Corned stations as a way of standardizing station

backlogs.

In addition to the sample inspection of specific non-outage work request tasks, the

team reviewed the existing non-outage backlog to determine distribution of the

backlog with respect to age and the station work group assigned responsibility for

closure. The following table is representative of the non-outage work request task

backlog for the powerblock that existed at the time of the inspection.

yROUP

1997

1996

1995

IM

98

25

5

EM

204

114

35

MM

208

163

33

FN

70

7

2

CFM

4

1

1

HVA

33

6

3

VM

29

134

44

MISC

31

15

3

TOTAL

677

465

126

TABLE NOTES

  • = 1993 or earlier for this column;

IM = instrument mechanics;

EM = electrical maintenance;

MM = mechanical maintenance;

FN = fix it now team;

1994

1

23

23

N/A

N/A

4

18

4

73

CFM = consolidated facility maintenance;

1993*

TOTAL

0

129

14

390

14

441

N/A

79

N/A

6

2

48

9

234

0

53

39

. 1380

=

HVA = heating ventilation and air conditioning maintenance team;

VM = valve maintenance team;

MISC = miscellaneous category with ten different sub-groups; and

N/A = not applicable .

39

The team reviewed the above backlog to evaluate the licensee's awareness of the

station's backlog of WR tasks and how those tasks were prioritized. The following

observations were made:

In general, the age of the existing backlog was skewed in a direction

indicating progress was being made at working off older items. The majority

(83 percent) of the non-outage backlog work request tasks were initiated in

1997 or 1996.

The licensee was emphasizing the oldest work request tasks through a

"Top 50" list that was intended to focus the responsible work group

attention. In addition, the ten oldest corrective tickets were specifically *

highlighted during the Plan of the Day meeting which was chaired by senior

station management.

The Plan of the Day meeting conducted a detailed review of the powerblock

backlog. The focus of that review, which included open WR and AR tasks,

was the station's weekly progress in completing scheduled work.

c.4

The licensee's knowledge of the current maintenance backlog was good. In

general, the maintenance backlog was appropriately coded so individuals

responsible for work prioritization had a sound data base. Some confusion in the

data base existed due to incorrectly coded work requests, and work tasks included

in the data base but actual field work was no longer required. The backlog of non-

outage work request tasks was skewed in a direction indicating positive progress

was being made at reducing the oldest backlog items and focusing attention on

more recent equipment deficiencies.

IV. Radiation Protection

R 1

Radiological Protection and Chemistry Controls

R 1 . 1 Actions to Control Licensed Radioactive Material within the Radiologically Protected

Area

a.

Inspection Scope (837501

The team reviewed the corrective actions specified in .licensee letter to the NRC

dated February 26, 1997, to prevent recurrence of the loss of control of licensed

radioactive material (RAM), in the form of contaminated articles, outside the

radiologically protected*area (RPA). The review consisted of interviews with plant

staff, observations of work in progress, walkdowns of the site, and review of

documentation .

40

,

b.

Observations and Findings

The team reviewed the survey log for dumpsters leaving the protected area from

January 24 through April 22, 1997, and noted that these surveys were conducted

, regularly with new meters designed to detect low levels of radioactivity. Radiation

protection technicians (RPTs) stated that only properly trained individuals were

allowed to conduct these surveys. The team observed that radworkers obtained

authorization from a radiation protection supervisor (RPS) before entering the RPA

with various work materials, and that the greeters quizzed the workers regarding

the need and authorization for this material. In addition, a review of the radiation

protection (RP) rover log revealed that rovers aided in the survey of items for

clearance from the RPA and raised housekeeping issues that had the potential to

result in the loss of control of contaminated materials.

The team reviewed the new stanchion control policy (Policy #71 ) which stated that

only yellow stanchions shall be used in the RPAs and green stanchions shall be

used in all others areas. The policy also stated that temporary satellite RPAs

(SRPAs) with smearable contamination items shall be surrounded by yellow

stanchions with a buffer zone of green stanchions surrounding the yellow

stanchions. During site walkdowns, the team noted that the stanchion policy was

well implemented. The team also observed the presence of a barrier on the second

floor of the Unit 2 side of the turbine building erected to separate the RPA and non-

RPA portions of the turbine building. Notes from the presentation given by the

radiation protection manager (RPM) at a site-wide meeting held on January 1 7,

1997, regarding the past problems with control of RAMs ~nd interviews with site

personnel indicated that control of RAM was effectively communicated.

The team interviewed RPS staff regarding a benchmarking visit to another nuclear

power plant. As a result of this visit, the RPS staff developed a satellite RPA

reduction plan to eliminate and consolidate the current 88 SRPAs into 30 SRPAs

after the Unit 3 outage. The team conducted an SRPA walkdown, interviewed the

lead RPS, and reviewed the SRPA reduction plan and noted that these actions

appeared adequate to address the recurrent problem of loss of control. The RP

staff also planned to establish a hot tool facility for the storage, use, and

decontamination of tools used in the RPA.

c.

Conclusion

The team concluded that some of the corrective actions to control licensed

radioactive material within site RPAs had been adequately implemented. Those

actions scheduled for implementation after the current Unit 3 outage appeared

sufficient to improve licensee performance in this area .

41

R 1.2 Actions to Effectively Control Access to High Radiation Areas

a.

Inspection Scope <837501

The team reviewed the status of corrective actions specified in licensee letter to the

NRC dated February 26, 1997, to prevent the recurrence of problems associated

with high radiation area (HRA) access. The review consisted of interviews with

plant staff, walkdowns within the RPA, and review of documentation.

b.

Observation and Findings

The team observed that the HRA keys were controlled and inventoried by RP staff.

Access to the HRA keys was limited to one RPT at the RP access control desk and

the inventory log was updated daily. Swing gates with proper postings were

located at the entrances to high radiatiOn areas throughout the plant, although the

alarms had not been installed. The team noted that greeters were not quizzing

radworkers about HRA controls and radworker responsibility. RPS staff stated that

greeter practice regarding HRA issues would be reviewed.

A RP staff survey of the HRA and locked HRA (LHRA) doors revealed 32 material

deficiencies. The lead technical health physicist was given the responsibility to

track and disposition the identified deficiencies. At the time of this inspection, six

  • HRAs were surveyed and downgraded to radiation areas, four areas were

downgraded from LHRAs to HRAs, and 26 of the 32 action requests written to

repair LHRA and HRA access points were complete. The team verified that the 2/3

maximum recycle demi.neralizer room LHRA door was locked.

Interviews with staff and a review of training notes from a presentation given by

the RPM to plant radworkers indicated that the workers were aware of

responsibilities and management expectations regarding work in HRAs. Regulatory,

TS, and procedural requirements were also communicated to the station

radworkers. RP and training staff stated that lesson plans addressing HRA issues

were being developed for integration into the operations, engineering, and

maintenance continuing training cycle.

c.

Conclusion

The team concluded that many of the.corrective actions had been implemented.

However, some training and repair issues remained incomplete. In addition, the

action to have greeters address HRA issues was not communicated to the greeters,

and was not being conducted.

R 1.3 Review of Refueling Outage Performance

a.

Inspection Scope

The team reviewed the licensee's radiological controls, dose and/or as low as

reasonably achievable (ALARA) effort, and work practices for the D3R 14 refueling

42

outage. The inspection consisted primarily of in-plant observations, attendance at

pre-job meetings, review of records (ALARA plans, radiation work permits (RWPs),

work packages, etc.), and discussions with workers and members of the work

control groups. The following radiologically significant jobs were inspected:

Reactor Water Cleanup (RWCU) Pipe Replacement

RWCU Removed Pipe and Heat Exchanger Shipping Activities

Removal of Waste Activities Associated with the RWCU

Refuel Floor Work Activities

Aspects of the Control Rod Drive (CRD) Removal Activities

Valve Work Activities

Drywall Work Activities

b.

Observations and Findings

As of May 2, 1997, the licensee had accrued about 118 rem (the projected goal for *

this period was 180 rem) with about fifty five percent of the scheduled work

completed. At that point, the overall outage dose was expected to be lower than

the original goal of about 300 rem (at the exit meeting on May 12, the licensee

informed the team that the goal for the Unit 3 outage had been reduced to

245 rem). To date, considerable work which had been included in the dose goal did

not need to be accomplished because many of the plant systems passed required

local leak rate tests (LLRTs). Added work scope, rework, and emergent work

accounted for about 40 rem, most of which was due to added scope. The outage

work scope growth was primarily due to work that was found to be required after

post shut down surveillances were performed.

ALARA controls such as mockup training, shielding, RWCU chemical

decontamination efforts, (the average decontamination factor was about 15), and

use of remote cameras and teledosimetry were implemented. Major outage

activities were assigned persons to be responsible for developing and implementing

the ALARA plans and ensuring radiological controls were used. Oversight by

radiation protection personnel and sufficient coordination between working groups

was observed. For those pre-job meetings attended, roles and responsibilities of

individuals were clearly discussed, and special instructions were prepared for those

jobs observed by the team. The team also observed the radiological controls

established for several jobs including the Unit 3 drywall, RWCU, and refuel floor

work activities. In addition, conservative radiological controls had been planned for

and were implemented for all work where there were indications of alpha

radioactivity.

43

c .

Although the radiation protection staff was observed to be aggressive in challenging

workers concerning loitering, knowledge of RWPs, general dose rates, and

monitoring requirements, the team observed some poor radworker practices that

could be prevented by closer oversight:

During the handling and loading of removed RWCU piping into transportation

bins, on two occasions, workers appeared to be loitering in general radiation

fields of 10 to 20 mrem per hour. Other workers were noted to be loitering

in radiation fields between the Unit 2 and Unit 3 door on the main floor in

radiation fields of about 6 mrem/hr.

Workers were instructed to perform a hand held frisk in a shielded booth* *

close to the RWCU work exit area, and then perform a whole body frisk

(PCM-18) at a lower elevation. On one occasion, the team observed four

workers exit the RWCU area, perform the hand held frisk, but only two of

the four performed the expected whole body frisk. On another occasion, the

team observed four workers exit the RWCU area, and neither a hand held

frisk or whole body frisk was performed.

These observations were discussed with the licensee, and RWCU work was

stopped until all persons associated with the project were instructed in licensee

expectations of worker performance.

Conclusions

The team concluded that, in general, radiological controls, ALARA initiatives, and

job planning were effectively implemented which contributed to the lower than

projected dose for the outage. Although some poor practices were observed,

overall, there was good effort to prevent loitering and unnecessary crew size.

R 1.4. Radiation Worker Practices

a.

Inspection Scope

The team observed general radiation work practices including personal monitoring,

use of protective clothing, dosimetry placement (thermolumenescent dosimetry

(TLDs) and electronic dosimeters (EDs)), working conditions, understanding general

and specific area dose rates and RWP requirements, and station housekeeping.

b.

Observations and Findings

The team observed. that the normal station practice was to put both the electronic

dosimeter (ED) and the theroluminescent dosimeter (TLD) in the same pocket with

both covered by the fabric of the PC. The team observed, on at least six

occasions, radiation workers placing their TLD or ED under protective clothing (PC),

and on two occasions the workers were radiation protection technicians .

44

...

Dresden Technical Specification 6.8.A required, in part, that written procedures

shall be implemented covering the activities referenced in Appendix A of Regulatory

Guide (RG) 1.33, "Quality Assurance Program Requirements (Operation),"

Revision 2, February 1978. Administrative and maintenance procedures were

referenced in RG 1 .33.

Dresden Administrative Procedure (OAP) 12-35, "Donning and Removal of Routinely

Required Radiological Protective Clothing Alli! PC Guidelines," Revision 4, Step F.1.j

required (unless otherwise directed by RWP QB Radiation Protection), that TLDs be

clipped to the PC pocket with the beta window showing and not covered by fabric,

and EDs were to be placed in the pocket. Failure to follow OAP 1 2-35 with regard

to the use of TLDs and EDs is another example of a Violation of TS 6.8.A

(50-237;249/97007-03d).

During a tour *of the sub-basement in the Unit 3 drywall, ladders and other debris

were observed almost blocking the entrance into the under-vessel area. The Unit 3

drywall coordinator removed the debris during the tour.

The team identified that packages of new piping insulation were staged in the

corner of the Unit 3 west LPCI corner room to support ongoing work. The

packages were radioactively clean and roped off in a noncontaminated area.

However a posted, radioactively contaminated trough ran along the base of the

floor and some piping insulation packages were laying across the contamination

boundary and in the contaminated trough. A radiation protection technician (RPT)

subsequently posted and controlled the area and as contaminated.

c.

Conclusions

The team concluded that most plant workers were adhering to acceptable

rad worker practices. However, the team concluded there were some instances of

poor procedural adherence or poor radworker practices.

V. Management Meetings

X 1

Exit Meeting Summary

The team discussed the progress of the inspection with licensee representatives on

\\ a daily basis and discussed inspection progress to members of licensee

management on April 25, 1997. A public exit meeting was held .on May 12, 1997.

In all cases, the _licensee acknowledged the findings presented.

45

PARTIAL LIST OF PERSONS CONTACTED

Licensee

  • S. Perry, Vice President, BWR Operations
  • J. Heffley, Units 2 and 3 Station Manager
  • F. Spangenburg, Regulatory Assurance Manager
  • P. Swafford, Unit 2/3 Maintenance Superintendent
  • R. Freeman, Site Engineering Manager
  • D. Winchester, Safety Quality Verification Director
  • T. Foster, Work Control and Outage Manager
  • c. Howland, Radiation Protection Manager
  • o. Willis, EMO Super"intendent
  • M. Milly, EMO General Supervisor
  • s. Stiles, IMO Superintendent

M. Pacilio, Outage Manager

S. Barrett, Operations Manager

  • R. Schultz,
  • c. Settles, State of Illinois, Resident Inspector
  • A. B. Beach, Regional Administrator, Riii
  • R. J. Caniano, Acting Director, Division of Nuclear Material Safety, Riii
  • G. E. Grant, Director, Division of Reactor Projects, Riii
  • J. A. Grobe, Acting Director Division of Reactor Safety, Riii
  • W. J. Kropp, Branch Chief, Division of Reactor Projects, Riii
  • P. L. Hiland, Branch Chief, Division of Nuclear Material Safety, Riii
  • K. R. Riemer, Senior Resident Inspector, Riii
  • C. E. Brown, Resident Inspector, Riii
  • o. E. Roth, Resident Inspector, Riii
  • R. A. Capra, Project Director, Division of Reactor Projects, NRR
  • Denotes those attending the May 12, 1997, exit meeting.

IP 71707

IP 61726

IP 62703

IP 62704

IP 62705

p 62707

LIST OF INSPECTION PROCEDURES USED

Operational .Safety Verification

Surveillance Testing

Maintenance Observations

Instrument Maintenance

Electrical Maintenance

Monthly Maintenance Observation

46

"

LIST OF ITEMS OPENED

Opened

50-237;249/97007-01

VIO

Failure to Follow Administrative and Test Procedures

During the Conduct of Instrument Maintenance

50-237;249/97007-02

VIO

Failure to Follow Instrument Surveillance Procedures

50-237;249/97007-03

VIO

Failure to Follow Administrative Procedures for FME

50-231;249/97007-04

VIO

Failure to Follow Mechanical Maintenance Procedures

During Welding

50-237;249/97007-05

VIO

Failure to Test 250 VDC Battery in As Found Condition

50-237;249/97007-06

VIO

Failure to Follow Administrative Controls for Procedural

Changes

A LARA

AR

ASME

ATS

ATWS

CAM

ccsw

CFR

Com Ed

CRD

cs

  • CST

D3R14

OAP

DCN

DDS

DES

DIP

DIS

DTI

ow

ECCS

ED

EM

E~D

EO

EWCS

LIST OF ACRONYMS USED

As Low As is Reasonably Achievable

Action Request

American Society of Mechanical Engineers

Analog Trip System

Anticipated Transient Without Scram

Continuous Air Monitor

Containment Cooling Service Water

. Code of Federal Regulations

Commonwealth Edison Company

Control Rod Drive

Core Spray

Control Systems Technician

Dresden Unit 3 Refueling Outage 14

Dresden Administrative Procedure

Design Change Notice

Dresden Electrical Surveillance

Dresden Electrical Surveillance

Dresden Instrument Procedure

Dresden Instrument Surveillance

Desk Top Instructions

Drywell

Emergency Core Cooling System

Electronic Dosimeter.

Electrical Maintenance

Electrical Maintenance Department

Environmental . Qualification

Electronic Work Control System

47

...

FIN

FME

FSAR

HCU

HPCI

HRA

IC

IEEE

IM

IMO

kV

LHRA

LLRT

LPCI

LPRM

MMD

M&TE

MOV

MPT

MSIV

MTU

NRC

NSWP

ace

oos

PDR

PIF

PORC

RG

RP

RPA

RPS

RPT

RPT/ARI

RWCU

RWP

S&LP

SBLC

SJAE

SRPA

SRM

STU

TLD

TS

voe

VPOP

WEC

WR

Fix it Now Team

Foreign Material Exclusion

Final Safety Analysis Report

Hydraulic Control Unit

High Pressure Coolant Injection

High Radiation Area

Instrument Controls

Institute of Electronic and Electrical Engineers

Instrument Mechanic

Instrument Maintenance Department

Kilovolts 4kV . = 4160 volt

Locked High Radiation Area

Local Leak Rate Test

Low Pressure Coolant Injection .

Local Power Range Monitor

Mechanical Maintenance Department

Maintenance and Test Equipment

Motor Operated Valve

Modified Performance Test

Main Steam Isolation Valve

Master Trip Unit

Nuclear Regulatory Commission

Nuclear Station Work Procedure

Outage Control Center

Out-of-Service

Public Document Room

Problem Identification Form

Plant Onsite Review Committee

Regulatory Guide

Radiation Protection

Radiologically Protected Area

Radiation Protection Supervisor

Radiation Protection Technician

Recirculation Pump Trip/Alternate Rod Insertion

Reactor Water Cleanup

Radiation Work Permit

Safety & Loss Prevention

Standby Liquid Control

Steam Jet Air Ejector

Satellite Radiologically Protected Area

Source Range Monitor

Slave Trip Unit

Thermoluminescent Dosimeter

Technical Specifications

Volts Direct Current

Valve Packing Optimization Program

Work Execution Center

Work Request 48

OAP 01-04 .

OAP 02-31

OAP 03-05

OAP 03-23

OAP 04-01

OAP 04-02

OAP 04-20

OAP 07-14

OAP 07-27

OAP 12-35

OAP 15-01

OAP 15-06

OAP 15-10

OAP 18-04

OAP 18-05

OAP 18-06

OAP 18-07

OAP 18-09

NSWP-WM-08

NSWP-WM-09

DIP 0700-08

DIS 0700-09

LIST OF DOCUMENTS REVIEWED

Contractor Controls

Electronic Work Control System (EWCS) Administration

Out of Service Program

Foreign Material Exclusion Program

Maintenance Department Organization

Dresden Preventive Maintenance Program Control

Calibration Program for M & TE/Standards

Operations Key Control

Independent verifications

Donning and Removal of Routinely Required Radiological Protective

Clothing and Protective Clothing Guidelines

Initiating and Processing a Work Request

Preparation, Approval, and Control of Work Packages and Work

Requests

Post Maintenance Testing Program

Management of Planned Outages

Shutdown Risk Assessment and Management

Long Range Planning

Implementation of the Fix it Now (FIN) Process

Work Activity Screening

Action Request Screening Process

Maintenance Work Scheduling Process Week E-5 to E + 1

SRM, IRM, and TIP Detector Resistance & Breakdown Voltage Checks

Preventative Maintenance and Calibration of IRM, SRM, RBM, LPRM

and APRM power supplies

49

..

DIS 0700-30

DIS 1500-14

DIS 2400-01

DES 8300-20

SRM/IRM Cable Routing and Detector Acceptance Test

LPCI System Discharge Header Flow Channel Calibration and Channel

Functional Test and Transmitter EO Maintenance Inspection

Post LOCA Containment H2/02 Analysis Functional/Calibration Test

Unit 3 250 vdc Station Battery Modified Performance Test

WR 950065509-01 Valve Flow Scans

WR 950070276-01 Main Condenser Expansion Boot Repair

WR 960096685-02 Welding in Torus

WR 960034393-01 H2/02 Monitor Repairs

WR 970002945-01 LPCI Master Trip Unit Calibration

WR 970032719-01 Calibration of H2/02 Monitors

WR 970042425-01 SRM Short Period Oscillations

WR 940097988-08 Unit 3 Replace Yarway Reactor Water Valve Switch

WR 950060521-01 D3 RFL EMO EQ GE 3A LPCI PMP MOTOR SURVEILLANCE

WR 960087265-01 2A MG Set Lube Oil Brg Oil Low Press Switch Vertical Mounting

Position and Calibration

WR 950062900-02 38 LPCI Cnmt Clg HX SW Outlet MOV Refurbishment and Calibration

WR 970001564-01 2A Off Gas Condenser Normal Level Control Malfunction

WR 960096144-01 2A Reactor Recirc MG Set Clamp MG Set Scoop Tube and Perform

DIS 0202-04

WR 970043047-01 Troubleshoot and Repair Unit 2 DW CAM Pegged Low

WR 970005193-01 D1, 2, 3, and 2/3 San PM River Temp Recorder Cal.

WR 960105540-01 U2 HPCI P*ump Suction from Condensate Storage Tank Check Valve

Disassembly and Inspection

WR 970041990-01 U2/3 Air Filtration Unit 4 Inch Charcoal Filter Halide Testing

WR 950060862-01 Bus 34 - Clean, Inspect Bus Bars, Wiring, Supports,

Insulation

50

.0

WR 950065566-01 U3 Main Steam Line C High Flow Isolation Non-TS

Surveillances

WR 960099060-01 Install Terminal Screws to ATWS Analog Trip System

Cabinet A

WR 970044365-01 Reinforce U2 Flued Head Anchor X-1168

Instrument Maintenance Task to Training Matrix

Instrument Maintenance Qualification Card 102

Instrument Maintenance Qualification Card 103

Unit 2, DIS 1600-03, Revision 07, "Torus to Reactor Building. Vacuum Relief Valves Trip

Unit Calibration" dated April 4, 1997

Unit 2, DIS 2400-02, Revision 10, "Post-LO CA Containment Hydrogen and Oxygen

Analyzer 18 Month Calibration and Maintenance Inspection" dated March 20, 1997

Unit 2/3, DIS 5700-04, Revision 0, "Reactor Building Vent Stack Flow Monitor Functional

Test" dated Aug 08, 1995

Unit 2, D'S 0263-07, Revision 08, "Unit 2 ATWS RPT/ARI and ECCS Level Transmitters

Channel Calibration Test and EQ Maintenance

Inspection" dated April 15, 1997

-

Unit 2, DIS 0250-01, Revision 14, "Main Steam Line High Flow Isolation Switch

Calibration" dated October 29, 1996

Unit 3, DIS 9900-01, Revision 07, "Computer Controlled Analysis Input Instrument

Calibration" dated April 17, 1997

Unit 2, DIS 0700-10, Revision 06, "Source Range Monitor (SRM) Rod Block Calibration"

dated January 31, 1997

Unit 3, DIS 5600-05, Revision 10, "Turbine Trips Functional Test (Not Tested in Another

Procedure)" dated February 14, 1996

Unit 2, DIS 2300-08, Revision 13, "Units 2/3 Contaminated Condensate Storage Tank and

Unit 2 Torus Level Switches Functional Test" dated March 6, 1997

Unit 2, DIS 0202-04, Revision 01, "Setting Recirculation Pump MG Set Scoop Tube

Control Rod Actuator Assembly Upper Mechanical and Electrical Stop" dated July 12,

1996

Unit 2, DIS 1700-17, Revision 05, "NMC Drywall Continuous Air Monitor Preventive

Maintenance and Calibration" dated December 18, 1996

51

Unit 2, DIS 1400-04, Revision 08, "Emergency Core Cooling System Fill System Alarm

Pressure Switches" dated February 04, 1997

Unit 2, DIS 0287-01, Revision 07, "Automatic Depressurization System CS and LPCI

Pumps Discharge Pressure - High (Permissive) Channel Calibration and Channel Functional

Test" dated April 07, 1997

Unit 2, DIS 1600-04~ Revision 14, "ECCS Drywell Pressure Switches Channel Calibration

and Channel Functional Test" dated March 21, 1997

Unit 3, DIP 0700-06, Revision 03, "LPRM Pre-Installation Insulation Resistance and

Breakdown Voltage Acceptance Checks" dated April 10, 1997

Unit 2, DIS 1600-10, Revision 16, "Drywall and Torus Pressure Instrumentation Channel

Calibration and EO Surveillance for Age Related Degradation" dated March 20, 1997

52