ML050450129

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IR 05000298-04-005, on 09/24/2004 - 12/31/2004, Cooper Nuclear Station, Fire Protection, ALARA Planning and Controls and Other Activities
ML050450129
Person / Time
Site: Cooper Entergy icon.png
Issue date: 02/14/2005
From: Hay M
NRC/RGN-IV/DRP/RPB-C
To: Edington R
Nebraska Public Power District (NPPD)
References
IR-04-005
Download: ML050450129 (30)


See also: IR 05000298/2004005

Text

February 14, 2005

Randall K. Edington, Vice

President-Nuclear and CNO

Nebraska Public Power District

P.O. Box 98

Brownville, NE 68321

SUBJECT:

COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION

REPORT 05000298/2004005

Dear Mr. Edington:

On December 31, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Cooper Nuclear Station. The enclosed integrated inspection report

documents the inspection findings which were discussed on January 6, 2005, with

Mr. S. Minahan, General Manager of Plant Operations, and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the NRC identified four findings that were evaluated

under the risk significance determination process as having very low safety significance

(Green). The NRC also determined that there were four violations associated with these

findings. However, because these violations were of very low safety significance and the issues

were entered into the licensees corrective action program, the NRC is treating these findings

as noncited violations (NCVs), consistent with Section VI.A.1 of the NRCs Enforcement Policy.

These NCVs are described in the subject inspection report. If you contest the subject or

significance of the NCVs, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive,

Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Cooper Nuclear Station facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response, if any, will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Nebraska Public Power District

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Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Michael C. Hay, Chief

Project Branch C

Division of Reactor Projects

Docket: 50-298

License: DPR-46

Enclosure:

NRC Inspection Report 05000298/2004005

w/attachment: Supplemental Information

cc w/enclosure:

Michael T. Boyce, Nuclear Asset Manager

Nebraska Public Power District

1414 15th Street

Columbus, NE 68601

John C. McClure, Vice President

and General Counsel

Nebraska Public Power District

P.O. Box 499

Columbus, NE 68602-0499

P. V. Fleming, Licensing Manager

Nebraska Public Power District

P.O. Box 98

Brownville, NE 68321

Michael J. Linder, Director

Nebraska Department of

Environmental Quality

P.O. Box 98922

Lincoln, NE 68509-8922

Chairman

Nemaha County Board of Commissioners

Nemaha County Courthouse

1824 N Street

Auburn, NE 68305

Nebraska Public Power District

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Sue Semerena, Section Administrator

Nebraska Health and Human Services System

Division of Public Health Assurance

Consumer Services Section

301 Centennial Mall, South

P.O. Box 95007

Lincoln, NE 68509-5007

Ronald A. Kucera, Deputy Director

for Public Policy

Department of Natural Resources

P.O. Box 176

Jefferson City, MO 65101

Jerry Uhlmann, Director

State Emergency Management Agency

P.O. Box 116

Jefferson City, MO 65102-0116

Chief, Radiation and Asbestos

Control Section

Kansas Department of Health

and Environment

Bureau of Air and Radiation

1000 SW Jackson, Suite 310

Topeka, KS 66612-1366

Daniel K. McGhee

Bureau of Radiological Health

Iowa Department of Public Health

401 SW 7th Street, Suite D

Des Moines, IA 50309

William J. Fehrman, President

and Chief Executive Officer

Nebraska Public Power District

1414 15th Street

Columbus, NE 68601

Jerry C. Roberts, Director of

Nuclear Safety Assurance

Nebraska Public Power District

P.O. Box 98

Brownville, NE 68321

Nebraska Public Power District

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Chief Technological Services Branch

National Preparedness Division

Department of Homeland Security

Emergency Preparedness & Response Directorate

FEMA Region VII

2323 Grand Boulevard, Suite 900

Kansas City, MO 64108-2670

Nebraska Public Power District

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Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (MRS)

Senior Resident Inspector (SDC)

Branch Chief, DRP/C (KMK)

Senior Project Engineer, DRP/C (WCW)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

RidsNrrDipmIipb

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

CNS Site Secretary (SLN)

NSIR/DPR/EPD (REK)

W. A. Maier, RSLO (WAM)

SISP Review Completed: _wcw___ ADAMS: / Yes

G No Initials: __wcw__

/ Publicly Available G Non-Publicly Available G Sensitive

/ Non-Sensitive

R:\\_CNS\\2004\\CN2004-05RP-SCS.wpd

RIV:RI:DRP/C

C:DRP/EB

C:DRS/OB

C:DRS/PSB

SDCochrum

SCSchwind

JAClark

ATGody

MPShannon

E - WCWalker

/RA/

/RA/

/RA/

/RA/

1/26/05

2/11/05

1/31/05

1/31/05

2/1/05

C:DRS/PEB

C:DRP/C

LJSmith

MCHay

/RA/

/RA/

1/29/05

2/14/05

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket.:

50-298

License:

DPR-46

Report:

05000298/2004005

Licensee:

Nebraska Public Power District

Facility:

Cooper Nuclear Station

Location:

P.O. Box 98

Brownville, Nebraska

Dates:

September 24 through December 31, 2004

Inspectors:

S. Schwind, Senior Resident Inspector

S. Cochrum, Senior Resident Inspector (temporary)

D. Carter, Health Physicist

P. Elkmann, Emergency Preparedness Inspector

G. Replogle, Senior Reactor Inspector

Approved By:

M. Hay, Chief, Branch C, Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000298/2004005; 09/24/04 - 12/31/04; Cooper Nuclear Station, Fire Protection, ALARA

Planning and Controls and other activities.

The report covered a 3-month period of inspection by resident inspectors and region-based

inspectors. Four Green noncited violations and one Green finding were identified. The

significance of the issues is indicated by their color (Green, White, Yellow, or Red) and was

determined by the significance determination process in Inspection Manual Chapter 0609.

Findings for which the significance determination process does not apply are indicated by the

severity level of the applicable violation. The NRC's program for overseeing the safe operation

of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight

Process, Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.d for failure to implement the stations fire watch procedure. Specifically, on

October 22, 2004, the inspectors identified that a compensatory fire watch,

responsible for protecting equipment important to safety from fire damage, was not

alert and therefore was inattentive to the areas assigned as directed by procedural

requirements.

This finding was considered more than minor since the finding would become a

more significant safety concern if left uncorrected. The finding was determined to

be of very low safety significance, since the finding was assigned a moderate fire

protection barrier degradation rating and did not degrade the automatic water-

based fire suppression system in the fire area. This finding had crosscutting

aspects associated with problem identification and resolution due to the licensees

failure to enter this condition into the corrective action program until prompted by

the inspectors approximately 10 days following its identification (Section 1R05).

Green. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, involving the failure to promptly identify and correct

conditions adverse to quality. Specifically, on numerous occasions the licensee

failed to promptly identify that environmental temperatures outside design

specifications could potentially affect the function of equipment important to

safety. As a result, the licensee failed to promptly evaluate this adverse condition

in a timely manner. The failure to promptly identify and correct this condition

adverse to quality involved crosscutting aspects associated with problem

identification and resolution.

The inspectors determined that the issue had more than minor safety significance

because it impacted the mitigating systems cornerstone objective and could have

affected the ability of safety-related systems to perform their design basis

functions. The finding was of very low risk significance because it was a

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Enclosure

design/qualification deficiency that did not result in a loss of function per Generic Letter 91-18, Information to Licensees Regarding NRC Inspection Manual Section

on Resolution of Degraded and Nonconforming Conditions, Revision 1

(Section 4OA5).

Cornerstone: Occupational Radiation Safety

Green. The inspectors identified a noncited violation of Technical Specification 5.7.1, since the licensee failed to barricade and conspicuously post a high

radiation area. On November 30, 2004, the inspector identified piping located in

the Residual Heat Removal B heat exchanger room that had dose rates elevated

to greater than 100 millirem per hour. The licensee performed a survey and

confirmed dose rates were 600 millirem per hour on contact with the pipe and

160 millirem per hour at 12 inches from the pipe. The area was immediately

barricaded and posted. The licensee entered this issue into its corrective action

program.

This finding is greater than minor because it was associated with the cornerstone

attribute (exposure control) and affected the cornerstone objective because failure

to post a high radiation area with dose rates greater than 100 millirem per hour

could increase the risk of personnel dosage. The finding was of very low safety

significance because it did not involve: (1) ALARA planning and controls, (2) an

overexposure, (3) a substantial potential for overexposure, or (4) an impaired

ability to assess dose (Section 2OS2).

Green. The inspector reviewed a self-revealing, noncited violation of Technical Specification 5.7.1 because the licensee failed to provide an individual a radiation

monitoring device that could be detected when a preset integrated dose alarm was

received. On December 15, 2003, an individual unknowingly exceeded the alarm

setpoint of a required electronic dosimeter while working in an area with radiation

levels as high as 200 millirem per hour. The electronic dosimeter was set to alarm

at 20 millirem, but upon exiting the area, the electronic dosimeter read 31 millirem

and was alarming. The individual did not hear the alarm until the area was exited.

The licensee entered this issue into its corrective action program.

This finding is greater than minor because it was associated with the cornerstone

attribute (exposure control) and affected the cornerstone objective because the

inability to detect an alarming device in a high radiation area could increase

personnel dose. The finding was of very low safety significance because it did not

involve: (1) ALARA planning and controls, (2) an overexposure, (3) a substantial

potential for overexposure, or (4) an impaired ability to assess dose. This finding

also had crosscutting aspects associated with human performance

(Section 2OS2).

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Enclosure

B.

Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee, have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

corrective actions are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

The plant was operating at full power at the beginning of this inspection period. On October 19,

2004, the reactor was shut down due to elevated main turbine rotor vibrations. Following repair

of the main turbine on November 10, 2004, full power operations resumed for the rest of the

inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

a.

Inspection Scope

The inspectors completed an inspection sample of licensee activities involving

preparations for cold weather conditions on two risk significant systems. These

activities included:

A review of maintenance work orders completed to prepare the systems for cold

weather conditions

A review of deficiency tags and condition reports associated with cold weather

protection measures to determine their impact on the systems

A walkdown of Emergency Diesel Generator (EDG) 2 to verify proper ventilation

alignments were implemented

A walkdown of the ventilation screens in the intake structure to verify that the

licensee had completed the required actions identified in the work orders

The two risk significant systems evaluated during this inspection included:

Portions of the EDG 2 system

The intake structure and environmental controls located in the service water pump

room

b.

Findings

No findings of significance were identified.

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Enclosure

1R04

Equipment Alignment (71111.04)

Partial Equipment Alignment Inspections

a.

Inspection Scope

The inspectors performed two partial equipment alignment inspections. The inspections

verified that critical portions of the selected systems were correctly aligned in

accordance with system operating procedures. The following two equipment alignment

inspections were performed:

EDG 1, while EDG 2 was inoperable during cleaning and coating of Diesel Fuel

Storage Tank 2 on October 25, 2004. The walkdown included accessible portions

of the system in the diesel generator room as well as temporary diesel fuel tanks,

hoses, and other equipment staged to support operability of EDG 1 during this

work. The inspectors also performed an as-found inspection of Diesel Fuel

Storage Tank 2 to assess its condition and an as-left inspection prior to refilling the

tank.

EDG 2, while EDG 1 was inoperable during cleaning and coating of the Diesel Fuel

Storage Tank 1 on November 1, 2004. The walkdown included accessible

portions of the system in the diesel generator room as well as temporary diesel

fuel tanks, hoses, and other equipment staged to support operability of EDG 2

during this work. The inspectors also performed an as-found inspection of Diesel

Fuel Storage Tank 1.

a.

Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

Quarterly Walkdowns

a. Inspection Scope

The inspectors performed six fire zone inspections to verify the licensee was maintaining

those areas in accordance with the fire hazards analysis. The fire zones were chosen

based on their risk significance as described in the individual plant examination of

external events. The walkdowns focused on control of combustible materials and

ignition sources, operability and material condition of fire detection and suppression

systems, and the material condition of passive fire protection features. The following

fire zones were inspected:

Fire Zone 1F/G, Control and computer rooms

Fire Zone 2A, Control rod mechanism North

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Enclosure

Fire Zone 3A/B, Critical switchgear room

Fire Zone 8D, Control Building Elevation 903

Fire Zone 8F/8G, Division 1 battery room and DC switchgear room

Fire Zone 20A/B, SW pump room

b.

Findings

Introduction. The inspectors identified a noncited violation (NCV) of Technical Specification (TS) 5.4.1.d for failure to implement the stations fire watch procedure.

Specifically, on October 22, 2004, the inspectors identified that a compensatory fire

watch, responsible for protecting equipment important to safety from fire damage, was

not alert and therefore was inattentive to the areas assigned as directed by procedural

requirements.

Description. On October 22, 2004, the inspectors conducted an inspection of the fire

protection features in the northeast section of the reactor building 903 level. The

inspectors identified that a compensatory fire watch, assigned to watch for fires in this

area, was not alert nor attentive to the area assigned. Following questioning by the

inspectors, the fire watch stated he was tired and therefore was not attentive to

assigned fire watch duties. The inspectors discussed the requirements of Administrative

Procedure 0.39, Fire Watches, Section 6.3.1, with the fire watch. The section states,

in part, that the fire watch shall observe the affected area and be alert for signs of fire,

smoke, and changing conditions. The inspectors then informed the shift manager and

outage manager who confirmed the fire watch appeared very tired and not alert and had

the watch relieved.

Analysis. The failure to implement the procedural requirements of Administrative

Procedure 0.39, Fire Watches, Revision 31, was considered a performance deficiency

which affected the mitigating systems cornerstone since compensatory fire watches are

used throughout the plant to protect safety-related equipment when fire protection

systems are degraded. This finding was considered more than minor since the finding

would become a more significant safety concern if left uncorrected. Inspection Manual

Chapter 0609, Significance Determination Process, Appendix F, was used to assess

the safety significance of this finding. Based on the results of a significance

determination process Phase 1 evaluation, the finding was determined to have very low

safety significance (Green) since the finding was assigned a moderate fire protection

barrier degradation rating and did not degrade the automatic water-based fire

suppression system in the fire area.

This finding had crosscutting aspects associated with problem identification and

resolution. This assessment was based on the fact that the licensee failed to enter this

condition into the corrective action program until prompted by the inspectors

approximately 10 days later.

Enforcement. TS 5.4.1.d states, Written procedures shall be established, implemented,

and maintained covering the fire protection program. Administrative Procedure 0.23,

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Enclosure

CNS Fire Protection Plan, Revision 41, Section 3.3, states, Fire Watches are

controlled by Procedure 0.39. Administrative Procedure 0.39, Fire Watches,

Revision 31, Section 6.3.1, states, in part, that the fire watch shall observe the affected

area and be alert for signs of fire, smoke, and changing conditions. Contrary to this

requirement, the fire watch failed to observe the affected area and remain alert to fire,

smoke, and changing conditions. Because this violation was of very low safety

significance and was entered into the corrective action program as Condition

Report CR-CNS-2004-07109, this violation is being treated as an NCV consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000298/2004005-01, Failure to

Implement the Station Fire Watch Procedure.

1R11 Licensed Operator Requalification (71111.11)

a.

Inspection Scope

On December 7, 2004, the inspectors observed one session of licensed operator

requalification training in the plant simulator. The training evaluated operator ability to

recognize, diagnose, and respond to a loss of dc power and a reactor scram.

Observations were focused on the following key attributes of operator performance:

Crew performance in terms of clarity and formality of communications

Ability to take timely and appropriate actions

Prioritizing, interpreting, and verifying alarms

Correct implementation of procedures, including the alarm response procedures

Timely control board operation and manipulation, including high-risk operator

actions

Oversight and direction provided by the shift supervisor, including the ability to

identify and implement appropriate TS requirements, reporting, emergency plan

actions, and notifications

Group dynamics involved in crew performance

The inspectors also verified that the simulator response during the training scenario

closely modeled expected plant response during an actual event.

b.

Findings

No findings of significance were identified.

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Enclosure

1R12

Maintenance Rule Implementation (71111.12)

a.

Inspection Scope

The inspectors reviewed one equipment performance issue to assess the licensees

implementation of their maintenance rule program. The inspectors verified that

components which experienced performance problems were properly included in the

scope of the licensees maintenance rule program and that the appropriate performance

criteria were established. Maintenance rule implementation was determined to be

adequate if it met the requirements outlined in 10 CFR 50.65 and Administrative

Procedure 0.27, Maintenance Rule Program, Revision 15. The inspectors reviewed

the following equipment performance problem:

Failure of breakers related to Lighting Panel EE-PNL- LPIS1 (CR 2004-07124)

b.

Findings

No findings of significance were identified

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a.

Inspection Scope

The inspectors reviewed two risk assessments for planned or emergent maintenance

activities to determine if the licensee met the requirements of 10 CFR 50.65(a)(4) for

assessing and managing any increase in risk from these activities. Evaluations for the

following maintenance activities were included in the scope of this inspection:

Corrective maintenance on the reactor core isolation cooling system to replace a

fuse and fuse holder on September 30, 2004 (CR 2004-06582)

Surveillance procedure on Residual Heat Removal (RHR) Loop B requiring

shutdown cooling to be secured on November 4, 2004 (Work Order 4360509)

b.

Findings

No findings of significance were identified.

1R14 Personnel Performance During Nonroutine Evolutions (71111.14)

a.

Inspection Scope

For the nonroutine event described below, the inspectors reviewed operator logs, plant

computer data, and strip charts to determine what occurred, how the operators

responded, and whether the response was in accordance with plant procedures.

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Enclosure

On October 18, 2004, the inspectors responded to the control room following

identification of elevated main turbine bearing vibrations. Based on the elevated

vibrations, operators performed a normal shutdown to inspect the main turbine

blades. The inspectors observed and evaluated the reactor shutdown, followup

actions by the operators, actions required by procedures, and monitoring of plant

conditions.

b.

Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed three operability determinations associated with mitigating

system capabilities to ensure that the licensee properly justified operability and that the

component or system remained available so that no unrecognized increase in risk

occurred. These reviews considered the technical adequacy of the licensees evaluation

and verified that the licensee considered other degraded conditions and their impact on

compensatory measures for the condition being evaluated. The inspectors referenced

the Updated Safety Analysis Report, TSs, and the associated system design criteria

documents to determine if operability was justified. The inspectors reviewed the

following equipment conditions and associated operability evaluations:

Reactor equipment cooling system leakage (CR 2004-06015)

Rod block monitor setpoint error (CR 2004-06893)

RHR Valve MO-13D failure to close (CR 2004-06776)

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope

The inspectors performed a review of all open operator workaround items to evaluate

their cumulative effect on mitigating systems and the operators ability to implement

abnormal or emergency procedures. In addition, open operability determinations and

selected condition reports were reviewed, and operators were interviewed to determine

if there were additional degraded or nonconforming conditions that could complicate the

operation of plant equipment.

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Enclosure

b.

Findings

No findings of significance were identified.

1R17

Permanent Plant Modifications

a.

Inspection Scope

The inspectors reviewed plant modification Change Evaluation Document (CED)

6008140 that replaced the reactor feedwater startup valves.

b.

Findings

Introduction. A Green self-revealing finding was identified involving the failure to

perform an adequate design change for the reactor feed system startup flow control

valves. The inadequate design change failed to ensure component temperature ratings

were not exceeded resulting in adversely affecting valve operation. Specifically, the

licensees evaluation failed to recognize and address acceptable O-ring types for the

temperatures of the reactor feed system.

Description. In September and October of 2004, several reactor feed pump (RFP)

trouble alarms, related to startup flow control valve abnormal operation, were received in

the control room. These valves are used to control feed water flow to the reactor vessel

during startup, cooldown, and depressurization. Based on initial testing and operation

following the alarms, the licensee determined that failed valve positioners were causing

the alarms. Both valve positioners were replaced September 25, 2004, however, during

testing the valves did not cycle as expected. During the investigation into the cause of

valve positioner failures, the licensee discovered the valve piston o-ring seal was

degraded, failing to provide the required seal. As a result, the valves would operate

erratically and deviate from normal demand.

The licensees apparent cause investigation discovered that the actuator O-rings were

square in shape indicating they had taken a permanent set due to exceeding the O-ring

temperature rating. The vendor manual states the temperature limit for this type of

actuator with nitrile O-rings is 175EF. During normal operation, the reactor feedwater

temperatures flowing thought the startup flow control valves reach as high as 360EF

exceeding the nitrile O-ring 175EF limit. In October of 2002, the licensee implemented

Modification CED 6008140, installing the inappropriate O-rings for the reactor feed

system startup flow control Valves RF-AOV-FCV11AA and RF-AOV-FCV11BB.

Analysis. The inadequate design review of the RFP startup flow control valve

modification (CED 6008140) was considered a performance deficiency, which affected

the Mitigating Systems cornerstone. This finding is greater than minor because it

affected both the Initiating Events and Mitigating Systems cornerstone attribute of

design control, reducing the reliability and capability of the RFP startup flow control

valves to mitigate events or potentially result in an initiating event based on loss of

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Enclosure

feedwater control to the reactor vessel. This issue is unresolved for significance

determination and the appropriate regulatory characterization (URI 05000298/2004005-

02, Review Safety Significance or Degraded Startup Flow Control Valves).

Enforcement. No violation of regulatory requirements occurred because the RFP

startup flow control valves are not classified as safety-related. The licensee entered this

finding into their corrective action program as Condition Report CR-CNS-2004-06997.

This finding is identified as FIN 05000298/2004005-02, Inadequate Design Review of

System Modification.

1R19 Postmaintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed or observed four selected postmaintenance tests (four

inspection samples) to verify that the procedures adequately tested the safety

function(s) that were affected by maintenance activities on the associated systems. The

inspectors also verified that the acceptance criteria were consistent with information in

the applicable licensing basis and design basis documents and that the procedures

were properly reviewed and approved. Postmaintenance tests for the following

maintenance activities were included in the scope of this inspection:

Emergency Diesel Generator 2 fuel oil pump replacement (Work Order 4376678)

Emergency Diesel Generator 2 fuel oil strainer cleaning and inspection (Work Order 4384984)

High pressure coolant injection exhaust drip leg drain extension (Work Order 4327601)

RHR system Valve RHR-MO-13D control switch replacement (Work Order 4406741)

b.

Findings

No findings of significance were identified.

1R20

Refueling and Outage Activities

a.

Inspection Scope

The inspectors observed outage-related activities during a forced outage following a

main turbine blade failure on October 18, 2004. Activities included reactor shutdown,

plant cooldown, placing the RHR system in the shutdown cooling mode of operation,

and startup activities.

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Enclosure

b.

Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors observed or reviewed the following four surveillance tests (four

inspection samples) to ensure that the systems were capable of performing their safety

function and to assess their operational readiness. Specifically, the inspectors verified

that the following surveillance tests met TS requirements, the Updated Safety Analysis

Report, and licensee procedural requirements:

6.HPCI.103, HPCI IST and 92 Day Test Mode Surveillance Operation,

Revision 26, performed on Oct 15, 2004

6.1DG.105, Diesel Generator Starting Air Compressor Operability (IST) (DIV 1),

Revision 13C1, performed on October 4, 2004

6.2RHR.706, RHR Loop B Injection Valve Time Delay Channel Functional Test

(DIV 2), Revision 2, performed on November 4, 2004

6.DWLD.302, Drywell Floor Drain Sump 1F Flow Loop Channel Calibration,

Revision 6, performed on December 14, 2004

b.

Findings

No findings of significance were identified.

Cornerstones: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

The inspector performed an in-office review of Revision 48 to the Cooper Nuclear

Station Emergency Plan, submitted October 20, 2004, and Revision 49 to the Cooper

Nuclear Station Emergency Plan, submitted October 25, 2004. This review included the

following changes that had been made to the plan:

Revised the physical description of installed meteorological instruments because

of replacement of the instruments, along with their associated ranges, tolerances,

and accuracy

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Enclosure

Revised the description of the emergency notification system from the Emergency

Broadcast System to the Emergency Alerting System, with associated details

related to system activation

Revised the location from which the emergency notification system is activated in

Atchinson County, Missouri, from the Sheriffs Department to the 911 Center

Revised the site emergency preparedness training guide from a guide document to

a procedure

Removed emergency preparedness from the site Quality Assurance for Operation

Policy Document

Revised the titles of several procedures.

The revision was compared to: its previous revision; the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1; the criteria of

ANSI/ANS-2.5-1984, American National Standard for Determining Meteorological

Information at Nuclear Power Sites; the criteria of Federal Emergency Management

Agency (FEMA) Report REP-10, Guide for the Evaluation of Alert and Notification

Systems for Nuclear Power Plants; and the requirements of 10 CFR 50.47(b) and

50.54(q) to determine if the revision decreased the effectiveness of the plan.

b.

Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a.

Inspection Scope

The inspectors observed the licensee perform one emergency preparedness drill on

December 9, 2004. Observations were conducted in the control room, technical support

center, and emergency operations facility. During the drill, the inspectors assessed the

licensees performance related to classification, notification, and protective action

recommendations. Following the drill, the inspectors reviewed the licensees critique to

determine if issues were appropriately identified and documented. The following

documents were reviewed during this inspection:

Emergency Plan for Cooper Nuclear Station

Emergency Plan Implementing Procedures for Cooper Nuclear Station

Cooper Nuclear Station Emergency Preparedness Drill Scenario for December 9,

2004

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Enclosure

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS2 ALARA Planning and Controls (71121.02)

a.

Inspection Scope

The inspector assessed licensee performance with respect to maintaining individual and

collective radiation exposures as low as is reasonably achievable (ALARA). The

inspector used the requirements in 10 CFR Part 20 and the licensees procedures

required by TSs as criteria for determining compliance. The inspector interviewed

licensee personnel and reviewed:

Current 3-year rolling average collective exposure

Three on-line maintenance work activities scheduled during the inspection period

and associated work activity exposure estimates which were likely to result in the

highest personnel collective exposures.

Site-specific trends in collective exposures, plant historical data, and source-term

measurements

Site-specific ALARA procedures

Intended versus actual work activity doses and the reasons for any inconsistencies

Integration of ALARA requirements into work procedure and radiation work permit

(or radiation exposure permit) documents

Person-hour estimates provided by maintenance planning and other groups to the

radiation protection group with the actual work activity time requirements

Shielding requests and dose/benefit analyses

Method for adjusting exposure estimates, or replanning work, when unexpected

changes in scope or emergent work were encountered

Use of engineering controls to achieve dose reductions and dose reduction

benefits afforded by shielding

Workers use of the low dose waiting areas

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Enclosure

Exposures of individuals from selected work groups

Declared pregnant workers during the current assessment period, monitoring

controls, and the exposure results

The inspector completed 8 of the required 15 samples and 5 of the optional samples.

b.

Findings

(1)

Introduction. The inspector identified an NCV of TS 5.7.1 for failure to barricade and

conspicuously post a high radiation area.

Description. On November 30, 2004, during walkdowns of the Reactor Building 931-foot

elevation, the inspector performed independent radiation measurements and identified

dose rates greater than 100 millirem per hour coming from RHR B heat exchanger

piping. This area was not posted and barricaded as a high radiation area, and it was

accessible from a scaffold platform. The radiation survey tag attached to the scaffold

ladder indicated general area dose rates of approximately 20 to 35 millirem per hour.

The licensee performed a survey of the area and confirmed dose rates of 600 millirem

per hour on contact with the pipe and 160 millrem per hour at one foot from the pipe.

The area was immediately barricaded and posted as a high radiation area.

Analysis. The failure to barricade and post a high radiation area is a performance

deficiency. This NRC-identified finding is greater than minor because it was associated

with a cornerstone attribute (exposure control), and affected the associated cornerstone

objective, to ensure the adequate protection of workers health and safety from

exposure to radiation, because not properly controlling high radiation areas could

increase personnel dose. The finding involved the potential for an individuals

unplanned or unintended dose, which could have been significantly greater as a result of

a single minor reasonable alteration of the circumstances. When processed through the

Occupational Radiation Safety Significant Determination Process, the finding was of

very low safety significance because it did not involve: (1) ALARA planning and

controls, (2) an overexposure, (3) a substantial potential for overexposure, or (4) an

impaired ability to assess dose.

Enforcement. TS 5.7.1 requires that each area in which radiation levels are in excess of

100 millirem per hour but less than 1000 millirem per hour shall be barricaded and

conspicuously posted as a high radiation area and entrance thereto shall be controlled

by requiring issuance of a specific work request. Contrary to this, the licensee failed to

barricade and post a high radiation area. Because the failure to barricade and post a

high radiation area was determined to be of very low safety significance and has been

entered into the licensees corrective action program as Condition Report CR-CNS-

2004-07496, this violation is being treated as an NCV consistent with Section VI.A of the

NRC Enforcement Policy: NCV 05000298/2004005-03, Failure to Barricade and Post a

High Radiation Area.

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Enclosure

(2)

Introduction. The inspector reviewed a self-revealing NCV of TS 5.7.1 for failure to

provide an individual a radiation monitoring device that could be detected when a preset

integrated dose alarm was received in a high radiation area.

Description. On December 15, 2003, an individual unknowingly exceeded the alarm

setpoint of a required radiation monitoring device (electronic dosimeter) while working in

an area with radiation levels as high as 200 millirem per hour. A worker exited the high

radiation area (the condenser area) with the electronic dosimeter in alarm. The workers

electronic dosimeter alarm was set at 20 millirem; upon exiting the area the electronic

dosimeter was reading 31 millirem. The worker did not hear the electronic dosimeter

alarm until the area was exited, and the alarm became self-revealing to the worker.

In addition to being unable to hear the electronic dosimeter alarm, the licensees

apparent cause determination identified that: (1) the worker failed to properly monitor his

dose during work, (2) the worker and the radiation protection technician failed to

communicate a specific stay time for a job, and (3) the radiation protection technician

failed to ensure the proper electronic dosimeter was used for the job, as required by the

radiation work permit.

Analysis. The failure to provide a radiation monitoring device that could be detected

when it alarms in a high radiation area is a performance deficiency. This self-revealing

finding is greater than minor because it was associated with a cornerstone attribute

(exposure monitoring), and affected the associated cornerstone objective, to ensure the

adequate protection of the workers health and safety from exposure to radiation,

because being unable to detect a radiation alarming device in a high radiation area

could increase personnel dose. The finding involved an individuals unplanned or

unintended dose. When processed through the Occupational Radiation Safety

Significant Determination Process, the finding was of very low safety significance

because it did not involve: (1) ALARA planning and controls, (2) an overexposure, (3) a

substantial potential for overexposure, or (4) an impaired ability to assess dose. The

finding also had crosscutting aspects associated with human performance.

Enforcement. TS 5.7.1 requires that any individual entering an area in which radiation

levels are in excess of 100 millirem per hour but less than 1000 millirem per hour shall

be provided with a monitoring device which continuously integrates the radiation dose in

the area and alarms when a preset integrated dose is received. Contrary to this, the

licensee failed to provide a monitoring device that can be detected when it alarms.

Because the failure to provide a radiation monitoring device that could be detected when

it alarms was determined to be of very low safety significance and has been entered into

the licensees corrective action program as Condition Report CR-CNS-2003-02009, this

violation is being treated as an NCV consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000298/2004005-04, Failure to Provide a Monitoring

Device that could Detect High Radiation in a Work Area.

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Enclosure

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

a.

Inspection Scope

The inspectors sampled two licensee PIs listed below for the period October 2003

through September 2004 (two inspection samples). The definitions and guidance of

Nuclear Energy Institute 99-02, Regulatory Assessment Indicator Guideline,

Revision 2, were used to verify that the licensee accurately reported PI data during the

assessment period. Licensee PI data was reviewed against the requirements of

Procedure 0-PI-01, Performance Indicator Program, Revision 16.

Reactor Safety Strategic Area

Reactor Coolant System Specific Activity

Reactor Coolant System Leak Rate

The inspectors reviewed a selection of licensee event reports, portions of operator log

entries, monthly reports, and PI data sheets to determine whether the licensee

adequately collected, evaluated, and distributed PI data for the period reviewed. The

inspectors also interviewed licensee personnel responsible for collecting and evaluating

PI data.

b.

Findings

No findings of significance were identified

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

The inspectors reviewed a selection of condition reports written during the inspection

period to verify the licensee was entering conditions adverse to quality into the

corrective action program at an appropriate threshold. Additionally, the inspectors

verified that condition reports were appropriately categorized and dispositioned in

accordance with the licensees procedures, and in the case of significant conditions

adverse to quality, to review the adequacy of licensee root cause determinations, extent

of condition reviews, and implemented corrective actions.

b.

Findings

No findings of significance were identified.

-15-

Enclosure

.2

Occupational Radiation Safety Sample Review

a.

Inspection Scope

The inspectors evaluated the effectiveness of the licensee's problem identification and

resolution processes regarding exposure tracking, higher than planned exposure levels,

and radiation worker practices. The inspector reviewed the corrective action documents

listed in the attachment against the licensees problem identification and resolution

program requirements.

b.

Findings

No findings of significance were identified.

.3

Semiannual Trend Review

a.

Inspection Scope

The inspectors performed a semiannual assessment of trends in the licensees

corrective action program to determine if any more significant safety issues exist.

Specifically, the inspectors reviewed the licensees corrective action program database

to determine if the licensee had identified trends in any of the following areas:

RFP controller alarms

Reactor equipment cooling leakage results

Intake structure silting

Contractor control

Average power range monitor alarms

Ronan computer multiplexer failures

345kv transformer alarms

120v ac lighting breaker tripping

Service air compressor failures

Procedure adherence

Operability determinations

These areas were chosen based on information gathered by the inspectors during the

previous 6 months. For those areas where trends were documented in the corrective

action program, the inspectors verified that the licensee had corrective actions planned

or in place to address the trend. For the remainder of the issues in the scope of this

inspection, the inspectors reviewed control room logs, system health reports, Quality

Assurance Audits, and department self-assessments and interviewed selected licensee

staff to determine if any adverse trends existed.

-16-

Enclosure

b.

Findings

The inspectors concluded that, in general, the licensee had adequately identified trends

in areas within the scope of this inspection; however, these trends were not always

explicitly documented in the corrective action program. This was a result of the

licensee's practice of closing new condition reports regarding similar equipment issues

to an existing condition report which was already open to evaluate the condition. In all

cases, the licensee was taking adequate corrective actions to address the trends.

There were six condition reports written during this 6-month period regarding lighting

panel breaker tripping related to Panel EE-PNL-LPIS1, which did not cross any

statistical thresholds in the licensee's trending program. The inspectors identified

several additional lighting breaker trips that were not documented in the correction

action program. During a discussion of these events, engineering personnel concluded

that a trend may exist. Condition Report CR-CNS-2004-07124 was written to document

a potential trend regarding breaker trips related to lighting Panel EE-PNL-LPIS1.

.4

Identification and Resolution of Problems Crosscutting Aspects of Findings

Sections 1R05 and 4OA5 describe findings with crosscutting aspects associated with

problem identification and resolution.

4OA4 Human Performance Crosscutting Aspects of Findings

Sections 1R17 and 2OS2 describe findings with crosscutting aspects associated with

human performance.

4OA5 Other Activities

(Closed) Unresolved Item 05000298/2004004-05: Plant temperatures outside Updated

Safety Analysis Report Limits

Introduction. The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion XVI, involving the failure to promptly identify and correct conditions adverse to

quality. Specifically, on numerous occasions the licensee failed to promptly identify that

environmental temperatures outside design specifications could potentially affect the

function of equipment important to safety. As a result, the licensee failed to promptly

evaluate this adverse condition in a timely manner. The failure to promptly identify and

correct this condition adverse to quality involved crosscutting aspects associated with

problem identification and resolution.

Description. The Cooper Updated Safety Analysis Report states, in part, that the design

of the station heating, ventilating, and air conditioning systems are based on a minimum

outdoor temperature of -5EF and a maximum outdoor temperature of 97EF. The

inspectors reviewed historical plant temperature data and noted that in the last 2 years

site temperatures had exceeded the 97 degree limit on 12 occasions and had dropped

-17-

Enclosure

below the -5EF threshold five times. During this same period plant temperatures were

as high as 104EF and as low as -10EF. Plant areas that directly rely on outside air for

temperature control during design basis accidents include the emergency diesel

generator rooms, portions of the reactor building, the control room, and the control

building.

The inspectors determined that engineering personnel failed to follow corrective action

program requirements resulting in the failure to promptly identify and correct a condition

adverse to quality. Specifically, although engineering was aware of the deviations from

the design temperature specifications, this nonconforming condition was not entered

into the corrective action program for resolution, resulting in the licensees failure to

evaluate the potential adverse affect to equipment being subjected to temperatures

outside design values.

Analysis. The inspectors determined that the issue had more than minor safety

significance because it impacted the mitigating systems cornerstone objective and could

have affected the ability of safety-related plant systems to perform their design basis

functions. The finding was of very low risk significance because it was a

design/qualification deficiency that did not result in a loss of function per Generic Letter 91-18, Information to Licensees Regarding NRC Inspection Manual Section on

Resolution of Degraded and Nonconforming Conditions, Revision 1.

This finding had crosscutting aspects associated with problem identification and

resolution. This assessment was based on the fact that the licensee failed to enter this

known nonconforming condition into the corrective action program.

Enforcement. The inspectors identified a violation of 10 CFR Part 50, Appendix B,

Criterion XVI (Corrective Actions), because the licensee had failed to properly identify

conditions adverse to quality. The noted regulation requires licensees, in part, to

promptly identify and correct conditions adverse to quality. Contrary to this requirement,

the inspectors identified 17 instances, in the last 2 years, where outside ambient

temperatures had exceeded design specifications for safety-related heating and

ventilation systems (conditions adverse to quality) and the licensee had failed to address

or evaluate the occurrences. Because the violation was of very low safety significance,

and was entered into the licensee's corrective action program (Condition Report 2004-

6820), this violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy (NCV 05000298/2004005-05).

4OA6 Meetings, Including Exit

On December 2, 2004, the inspectors presented the ALARA Planning and Controls

inspection results to Mr. S. Minahan, General Manager of Plant Operations, and other

members of his staff who acknowledged the findings.

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Enclosure

On December 13, 2004, the inspectors conducted a telephonic exit meeting of the

emergency preparedness inspection results to Mr. J. Bednar, Emergency Preparedness

Manager, and other members of his staff who acknowledged the findings.

On January 6, 2005, the inspectors presented the results of the resident inspector

activities to Mr. S. Minahan, and other members of his staff, who acknowledged the

findings.

The inspectors confirmed that proprietary information was not provided or examined

during the inspection.

40A7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meet the criteria of Section VI of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

Cornerstone: Barrier Integrity

TS 5.6.5(a)3 required the licensee to determine the rod block monitor upscale

allowable values and document the values in the core operating limits report

prior to each reload cycle. Contrary to this requirement, this determination was

not completed prior to Reload Cycle 22. The licensee used generic values

provided by the vendor vice determining cycle-specific values. This resulted in

nonconservative rod block monitor upscale setpoints. This finding affected the

Barrier Integrity cornerstone and was of very low safety significance since it did

not represent an actual degradation of a fission product barrier. This was

identified in the licensees corrective action program as Condition Report CR-

CNS-2004-06893.

ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

J. Bednar, Emergency Preparedness Manager

C. Blair, Engineer, Licensing

D. Cook, Technical Assistant to General Manager

J. Christensen, Co-Director of Nuclear Safety Assurance

S. Minahan, General Manager of Plant Operations

T. Chard, Radiological Manager

K. Chambliss, Operations Manager

K. Dalhberg, General Manager of Support

J. Edom, Risk Management

R. Estrada, Corrective Actions Manager

J. Flaherty, Site Regulatory Liaison

P. Fleming, Licensing Manager

D. Knox, Maintenance Manager

W. Macecevic, Work Control Manager

J. Roberts, Director, Nuclear Safety Assurance

R. Shaw, Shift Manager

J. Sumpter, Senior Staff Engineer, Licensing

K. Tanner, Shift Supervisor, Radiation Protection

R. Hayden, Emergency Preparedness Staff

NRC Personnel

L. Ricketson, Senior Health Physicist

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000298/2004005-02

URI

Review Safety Significance of Degraded Startup Flow

Control Valves (Section 1R17)

Opened and Closed

05000298/2004005-01

NCV

Failure to Implement the Station Fire Watch Procedure

(Section 1R05)05000298/2004005-03

NCV

Failure to barricade and conspicuously post a high radiation

area (Section 2OS2)

A-2

Attachment

05000298/2004005-04

NCV

Failure to provide a radiation monitoring device that could

detect high radiation in a work area (Section 2OS2)05000298/2004005-05

NCV

Plant Temperatures Outside Design Specifications

(Section 4A05)

Closed

05000298/2004004-05

URI

Plant temperatures outside Updated Safety Analysis Report

limits (Section 4A05)

LIST OF DOCUMENTS REVIEWED

Condition Reports

2004-06045

2004-06015

2004-07124

2004-06567

2004-06582

2004-06757

2004-06835

2004-07120

Section 2OS2: ALARA Planning and Controls (71121.02)

Corrective Action Documents

2003-1787, 2003-61136, 2003-7706, 2004-1699, 2004-5224, 2004-5969, 2004-5970, 2004-

5973, 2004-6327, and 2004-6360 and 10299462 and 10314221

Audits and Self-Assessments

Snap Shot Assessment dated July 19-23, 2004

Snap Shot Assessment dated May 24, 2004

Snap Shot Assessment dated June 2, 2004

Radiation Work Permits

2003-1111

Condenser tube leak and repair

2004-1047

Condenser water box cleaning

2004-1050

Fan B cooling unit bearing replacement

Procedures

0.ALARA.1

CNS ALARA Program, Revision 3

0.ALARA.2

ALARA Organization and Management, Revision 7

9.ALARA.4

Radiation Work Permits, Revision 4

9.RADOP.3

Area Posting and Access Control, Revision 16

9.ALARA.1

Radiation Protection at CNS, Revision 4

9.ALARA.5

ALARA Planning and Controls, Revision 12

9ALARA.12

Hot Spot Reduction Program, Revision 0

9.EP 3.14

Temporary Shielding, Revision 15

ALARA Committee Meeting Minutes

2003

February 19, 2003

June 6, 2003, ALARA Special Committee Meeting Minutes

1st Quarter 2003

3rd Quarter 2003

September 11, 2003, Water Box Cleaning

4th Quarter 2003

2004

2004-02, 2004-03, 2004-04, 2004-05, 2004-06, 2004-07, 2004-08, 2004-09, 2004-10, 2004-11,

2004-12, and 2004-13

Miscellaneous

2003 ALARA Program and RE21 Review

LIST OF ACRONYMS

ALARA

as low as is reasonably achievable

CED

change evaluation document

CFR

Code of Federal Regulations

EDG

emergency diesel generator

FIN

finding

NCV

noncited violation

NRC

U.S. Nuclear Regulatory Commission

PI

performance indicator

RFP

reactor feed pump

RHR

residual heat removal

TS

Technical Specification

A-3

Attachment