ML041120590

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IR 05000254-04-002, 05000265-04-002, on 01/01/2004 - 03/312004, Quad Cities Nuclear Power Station Units 1 & 2, Cordova, Il; Event Followup
ML041120590
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 04/19/2004
From: Ring M
NRC/RGN-III/DRP/RPB1
To: Crane C
Exelon Generation Co
References
IR-04-002
Download: ML041120590 (57)


See also: IR 05000254/2004002

Text

April 19, 2004

Mr. Christopher M. Crane

President and Chief Nuclear Officer

Exelon Nuclear

Exelon Generation Company, LLC

Quad Cities Nuclear Power Station

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000254/2004002;

05000265/2004002

Dear Mr. Crane:

On March 31, 2004, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed report

documents the inspection findings which were discussed on April 6, 2004, with Mr. Tulon and

other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and to

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the inspectors identified one finding of very low safety

significance (Green) which was determined to involve a violation of NRC requirements.

However, because this violation was of very low safety significance and because it was entered

into your corrective program, the NRC is treating this finding as a Non-Cited Violation in

accordance with Section V1.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulation Commission, ATTN: Document Control Desk, Washington, DC

20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the

Resident Inspector Office at the Quad Cities Nuclear Power Station.

C. Crane

-2-

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-254; 50-265

License Nos. DPR-29; DPR-30

Enclosure:

Inspection Report 05000254/2004002; 05000265/2004002

w/Attachment: Supplemental Information

cc w/encl:

Site Vice President - Quad Cities Nuclear Power Station

Plant Manager - Quad Cities Nuclear Power Station

Regulatory Assurance Manager - Quad Cities Nuclear Power Station

Chief Operating Officer

Senior Vice President - Nuclear Services

Senior Vice President - Mid-West Regional

Operating Group

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing - Mid-West Regional

Operating Group

Manager Licensing - Dresden and Quad Cities

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

Vice President - Law and Regulatory Affairs

Mid American Energy Company

Assistant Attorney General

Illinois Department of Nuclear Safety

State Liaison Officer, State of Illinois

State Liaison Officer, State of Iowa

Chairman, Illinois Commerce Commission

D. Tubbs, Manager of Nuclear

MidAmerican Energy Company

DOCUMENT NAME: G:\\quad\\ML041120590.wpd

To receive a copy of this document, indicate in the box:"C" = Copy without enclosure "E"= Copy with enclosure"N"= No copy

OFFICE

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NAME

MRing for

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DATE

04/19/04

04/19/04

OFFICIAL RECORD COPY

C. Crane

-3-

ADAMS Distribution:

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HBC

KKB

C. Ariano (hard copy)

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-254; 50-265

License Nos:

DPR-29; DPR-30

Report No:

05000254/2004002; 05000265/2004002

Licensee:

Exelon Nuclear

Facility:

Quad Cities Nuclear Power Station, Units 1 and 2

Location:

22710 206th Avenue North

Cordova, IL 61242

Dates:

January 1 through March 31, 2004

Inspectors:

K. Stoedter, Senior Resident Inspector

M. Kurth, Resident Inspector

S. Caudill, Resident Inspector - Duane Arnold

J. House, Senior Radiation Specialist

D. Jones, Reactor Engineer

D. Nelson, Radiation Specialist

L. Ramadan, Nuclear Safety Intern

R. Ganser, Illinois Emergency Management Agency

Approved by:

M. Ring, Chief

Branch 1

Division of Reactor Projects

Enclosure

1

SUMMARY OF FINDINGS

IR 05000254/2004002, 05000265/2004002; 01/01/2004-03/31/2004; Quad Cities Nuclear

Power Station, Units 1 & 2; Event Followup.

This report covers a 3-month period of baseline resident inspection and announced baseline

inspections on inservice inspection and radiation protection. The inspection was conducted by

Region III inspectors and the resident inspectors. One Green finding involving one Non-Cited

Violation was identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green. A finding of very low safety significance was self-revealed when a radiation

protection technician performing surveys in the Unit 1 drywell discovered that the 3B

electromatic relief valve pilot valve vent line was broken off at the pilot valve chamber

assembly. The pilot valve vent line broke due to the failure to have standard instructions

to identify, evaluate, and resolve issues related to cold spring forces during the

installation of small-bore piping. Over time the cold spring forces, taken in conjunction

with the increased vibrations caused by the extended power uprate, led to a condition

where the electromatic relief valve (an automatic depressurization system valve) would

not have operated when called upon. Corrective actions for this issue included

informing maintenance personnel of potential cold-spring issues during piping

installations, repairing the 3B electromatic relief valve, and inspecting the remaining

relief valves for similar degradation.

This finding was more than minor because the inoperability of one of the automatic

depressurization system valves impacted the overall operability, availability, and

reliability of the automatic depressurization system which can be utilized following a

small break loss of coolant accident. This finding was of very low safety significance

since operations personnel could have manually depressurized the reactor vessel if

needed and all other mitigating systems equipment was available. This finding was

determined to be a Non-Cited Violation of Technical Specifications 3.4.3.A and 3.5.1.G

due to having an automatic depressurization system valve inoperable for greater than

14 days. (Section 4OA3)

B.

Licensee-Identified Violations

No findings of significance were identified.

Enclosure

2

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period with reactor power administratively limited to 85 percent

pending the evaluation of extended power uprate vibration data and the affects of these

vibrations on plant equipment. Short duration power reductions were conducted on

February 22 and March 14 in order to perform turbine valve testing and control rod scram time

testing. Unit 1 operated at 85 percent power for the remainder of the inspection period.

Unit 2 began the inspection period operating at 96 percent power. During the month of

January, operations personnel performed two planned power reductions to perform control rod

pattern adjustments. On February 2, operations personnel reduced reactor power to

approximately 55 percent due to a high pressure feedwater heater relief valve actuation.

Maintenance personnel replaced the relief valve which allowed operations personnel to return

Unit 2 to 96 percent power on February 3. Refueling outage Q2R17 began on February 24.

Major activities performed during the outage included replacing the low pressure turbine

buckets, chemical decontamination of reactor recirculation system piping, noble metals

injection, replacing the power operated relief valves with electromatic relief valves, installing a

digital reactor recirculation control system, and installing a new main power transformer.

Operations personnel commenced startup activities on March 27. Unit 2 was sychronized to

the electrical grid the following day. Approximately two days later, a reactor scram occurred

during routine turbine thrust bearing wear detector testing. After completing repairs, the

licensee commenced a second reactor startup the evening of March 30. At the end of the

report period the licensee was at 70 percent power and continuing with power ascension

activities.

1.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01

Adverse Weather (71111.01)

a.

Inspection Scope

In early January, Quad Cities Station experienced outside air temperatures below

0 degrees. In preparation for the extreme cold, engineering personnel informed the

operations department that the contaminated condensate storage tank heater breakers

would likely begin to trip due to internal shorting caused by entrained moisture. The

inspectors selected this actual adverse weather condition for additional inspection

because if the water in the tank froze, the normal suction source to the high pressure

coolant injection, reactor core isolation cooling, and safe shutdown makeup systems

would be lost. In addition, safety-related instrumentation inside the tank which ensured

that the mitigating systems listed above were supplied by an alternate suction source

under low tank level conditions may be lost.

The inspectors reviewed the Updated Final Safety Analysis Report and engineering

Enclosure

3

calculations to determine the actual number of heaters needed to prevent the

contaminated condensate storage tanks from freezing. The licensees cold weather

procedures were reviewed to determine if the tank heater breakers were inspected on a

periodic basis. The inspectors interviewed operations and engineering personnel to

determine the tank heater breakers equipment history, the actions taken previously to

prevent the breakers from tripping, and to become familiar with the temporary

modifications installed to ensure that the required number of tank heaters remained

energized. Lastly, the inspectors reviewed several condition reports associated with the

breaker trips.

b.

Findings

No findings of significance were identified. However, problem identification and

resolution observations associated with this issue can be found in Section 4OA2 of this

report.

1R04

Equipment Alignment (71111.04)

a.

Inspection Scope

The inspectors performed partial walkdowns of the following four risk-significant

mitigating systems equipment during times when the equipment was of increased

importance due to redundant systems or other equipment being unavailable:

Unit 1 High Pressure Coolant Injection;

Unit 2 Core Spray;

Unit 2 Fuel Pool Cooling; and

Unit 2 Reactor Building Closed Cooling Water.

The inspectors utilized the valve and breaker checklists listed at the end of this report to

verify that the components were properly positioned and that support systems were

aligned as required. The inspectors examined the material condition of the components

and observed equipment operating parameters to verify that there were no obvious

deficiencies. The inspectors reviewed outstanding work orders and condition reports

associated with each system to verify that those documents did not reveal issues that

could affect the equipment inspected. The inspectors compared the information in the

appropriate sections of the Updated Final Safety Analysis Report to actual equipment

performance data to determine that the system was capable of performing its design

function. Lastly, the inspectors reviewed Condition Reports 205146, 205514, 205862,

205892, 205902, 205908, 205910, and 206471 which were initiated during the

inspection to ensure that the inspectors observations were adequately documented and

that appropriate corrective actions were implemented.

b.

Findings

No findings of significance were identified.

Enclosure

4

1R05

Fire Protection (71111.05)

.1

Quarterly Fire Zone Walkdowns

a.

Inspection Scope

The inspectors performed routine walkdowns of accessible portions of the following risk

significance fire zones:



Fire Zone 1.1.1.6 - Refuel Floor;



Fire Zone 1.2.2 - Unit 2 Drywell;



Fire Zone 8.2.6.D - Unit 2 Low Pressure Heater Bay;

Fire Zone 8.2.6.E - Unit 2 High Pressure Heater Bay;

Fire Zone 8.2.7.D - Unit 2 Low Pressure Heater Bay West;

Fire Zone 8.2.8.A - Unit 1 Switchgear Area; and

Fire Zone 8.2.8.E - Unit 2 Turbine Deck.

During a walkdown of each fire zone, the inspectors verified that transient combustibles

were controlled in accordance with the licensees procedures and observed the physical

condition of fire suppression devices. The inspectors verified the condition and

placement of fire extinguishers and hoses against the Pre-Fire Plan fire zone maps.

The physical condition of accessible passive fire protection features such as fire doors,

fire dampers, fire barriers, fire zone penetration seals, and fire retardant structural steel

coatings were also inspected to verify proper installation and physical condition.

b.

Findings

No findings of significance were identified.

.2

Annual Fire Drill Observation

a.

Inspection Scope

The inspectors observed the fire brigade participate in fire drills on January 28 and

February 3. The simulated fires occurred on the turbine deck within one of the reactor

recirculation motor generator sets. These fire drills were chosen because the fire

hazard location was adjacent to safety-related switchgear needed to safely shut down

the plant during certain fire scenarios. The inspectors observed that protective clothing

was properly donned; self-contained breathing apparatus equipment was properly worn

and used; fire hose lines were capable of reaching the necessary fire hazard locations;

the fire area was entered in a controlled manner; sufficient fire fighting equipment was

brought to the scene; the fire brigade leaders fire fighting directions were thorough,

clear, and effective; fire fighting pre-planned strategies were utilized; the licensees

pre-planned drill scenario was followed, and the drill objectives acceptance criteria were

met. The inspectors also reviewed Condition Report 204252 which was written to

document weaknesses identified by the licensee during the first quarter 2004 fire drills.

Enclosure

5

b.

Findings

No findings of significance were identified.

1R07

Heat Sink (71111.07A)

a.

Inspection Scope

On February 10, the inspectors observed engineering and operations personnel

complete performance testing on the 2A residual heat removal heat exchanger. This

heat exchanger was chosen for inspection due to its high safety significance and risk

significance. During the testing observation the inspectors verified that the acceptance

criteria and test results considered differences between test and design basis conditions

because testing at the design heat removal rate was not practical. The inspectors also

performed independent calculations using the licensees test results to confirm that the

results considered possible uncertainties and that the heat exchanger remained capable

of performing its safety function.

b.

Findings

No findings of significance were identified.

1R08

Inservice Inspection Activities (71111.08)

a.

Inspection Scope

The inspectors conducted a review of the implementation of the licensees inservice

inspection program for monitoring degradation of the Unit 2 (Q2R17 Outage) reactor

coolant system boundary and the risk significant piping system boundaries.

Specifically, the inspectors conducted a (onsite or record) review of the following five

nondestructive examination activities to evaluate compliance with the American Society

of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code requirements and to

verify that indications and defects were dispositioned in accordance with the ASME

Code: (This review counted as two samples.)

Ultrasonic examination of reactor core isolation cooling system elbow to pipe

weld IRI-1002-16;

Ultrasonic examination of feedwater system pipe to elbow weld 1FW-1001-68;

Ultrasonic examination of residual heat removal system pipe to elbow weld

1RH-1004-24;

Magnetic particle examination of residual heat removal heat exchanger shell to

saddle fillet weld N6A-F1; and

Magnetic particle examination of residual heat removal heat exchanger shell to

nozzle fillet weld N6A-F2.

The inspectors also reviewed the following examination from the previous outage

(Q1R17) with recordable indications that has been accepted by the licensee for

Enclosure

6

continued service to verify that the licensees acceptance for continued service was in

accordance with the ASME Code: (This review counted as one sample.)

Recordable indications found during visual examination of jet pumps #2 and #7

AD-3b welds.

The inspectors reviewed pressure boundary welds for Class 1 or 2 systems which were

completed since the beginning of the previous refueling outage, to verify that the

welding acceptance (e.g., radiography) and pre-service examinations were performed in

accordance with ASME Code requirements: (This review could not be counted as a

sample.)

This review found that no pressure boundary welds for Class 1 or 2 systems

were completed since the beginning of the previous refueling outage.

The inspectors reviewed one ASME Section XI Code repair or replacement to verify the

repair and replacement met ASME Code requirements. (This review counted as one

sample.)

Main steam system ASME Section XI, 1989 Edition, Code Class 1 snubber

replacement and addition of new welds (W.O. 99242365-22).

The inspectors reviewed a sample of inservice inspection-related problems documented

in the licensees corrective action program to assess conformance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. In addition, the inspectors

verified that the licensee correctly assessed operating experience for applicability to the

inservice inspection group.

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk and Emergent Work (71111.13)

a.

Inspection Scope

The inspectors reviewed the documents listed in the List of Documents Reviewed

section of this report to determine if the risk associated with the listed activities agreed

with the results provided by the licensees risk assessment tool. In each case the

inspectors conducted walkdowns to ensure that redundant mitigating systems and/or

barrier integrity equipment credited by the licensees risk assessment remained

available. When compensatory actions were required, the inspectors conducted plant

inspections to validate that the compensatory actions were appropriately implemented.

The inspectors also discussed emergent work activities with the shift manager and work

week manager to ensure that these additional activities did not change the risk

assessment results.

Enclosure

7

Work Week January 26 through 31, including planned maintenance or

suveillance testing on the Unit 1 emergency diesel generator, the Unit 1 reactor

core isolation cooling system, and emergent work on the Unit 2 essential service

bus uninterruptable power supply;

Work Week February 9 through 14, including planned maintenance on the 1A

and 1B residual heat removal service water pumps, the 1A and 1B residual heat

removal pumps, the Unit 1 station blackout diesel generator, and emergent work

on a Unit 2 residual heat removal service water pump;

Work Week February 16 through 21, including planned maintenance on the 2A

control rod drive pump, the 2B electrohydraulic control pump, the 2A stator water

cooling pump, and one of the Unit 2 bus duct blowers;

Work Week February 23 through 28, including planned maintenance on bus 23,

bus 24, bus 24-1, bus 25, bus 27, bus 29, motor control center 29-2, the 1/2A

standby gas treatment system, the Unit 2 emergency diesel generator, the Unit 2

250 Vdc battery, and Unit 2 250 Vdc bus 2A; and

Work Week March 8 through March 13, including planned maintenance on

bus 23, bus 23-1, the 1/2 emergency diesel generator, the 1/2A standby gas

treatment system, and various breakers.

b.

Findings

No findings of significance were identified.

1R14

Non-Routine Evolutions (71111.14)

.1

Failure of High Pressure Feedwater Heater Relief Valve

a.

Inspection Scope

During the week of February 2, the inspectors reviewed Technical Specifications,

procedures, control room log entries, maintenance work orders, condition reports, and

interviewed licensee personnel to determine the circumstances that led to the failure of

a high pressure feedwater heater relief valve and a corresponding power reduction. The

results of this review were used to verify that operations personnel had responded to the

relief valve failure as required by procedures. The inspectors also reviewed several

condition reports previously written on the feedwater heater relief valves to ensure that

the failure was not a repeat condition and that prior corrective actions were appropriate

to the circumstance.

b.

Findings

No findings of significance were identified.

Enclosure

8

.2

Unit 2 Reactor Scram During Turbine Valve Testing

a.

Inspection Scope

The inspectors observed operator performance in coping with the Unit 2 turbine trip and

subsequent reactor scram while conducting turbine testing on March 30, 2004. In

particular, operators were testing the turbine thrust bearing wear detector when the

turbine trip occurred. The inspectors reviewed operator logs and plant computer data.

Also, the inspectors evaluated the operators response to ensure it was in accordance

with station procedures and training.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors assessed the following operability evaluations or condition reports

associated with equipment operability issues:

Condition Report 179235, Potentially Nonconservative Pressure Temperature

Curves;

Condition Report 148103, Nonconforming Moore Industries SCT Signal

Converter/Isolator;

Condition Report 191530, 125 Volt DC Grounds Identified on Power Operated

Relief Valves 2-0203-3B and 2-0203-3E;

Condition Report 131936, Missing Belleville Washer in 1-0203-2C Main Steam

Isolation Valve;

Condition Report 132397, Manufacturing Deficiency in Agastat Model ETR

Relays;

Condition Reports 205862 and 205892, Wrong Oil in the 2A and 2B Core Spray

Pump Motors; and

Condition Report 200772, Main Steam Safety Valves May Not Have Met

Technical Specification Requirements.

The inspectors reviewed the technical adequacy of the evaluation against the Technical

Specifications, Updated Final Safety Analysis Report, and other design information;

determined whether compensatory measures, if needed, were taken; and determined

whether the evaluations were consistent with the requirements of LS-AA-105,

Operability Determination Process. The inspectors also reviewed selected issues that

the licensee entered into its corrective action program to verify that identified problems

were being entered into the program with the appropriate characterization and

significance.

Enclosure

9

b.

Findings

During the review of a Technical Specification amendment request for Dresden Station,

the Office of Nuclear Reactor Regulation identified a concern regarding the ability of the

main steam safety valves to meet Technical Specification Surveillance

Requirement 3.4.3.1. Technical Specification Surveillance Requirement 3.4.3.1

required the licensee to demonstrate that the main steam safety valves lifted within plus

or minus one percent of the setpoint assumed in the reactor overpressure analysis and

the anticipated transient without scram overpressure analysis.

Quad Cities engineering personnel reviewed the NRCs concern and identified that a

similar condition existed at the station. A review of historical as-found main steam

safety valve testing results determined that some of the valves operated outside of the

one percent tolerance specified in the Technical Specifications. As a result, the licensee

may not have been able to ensure that a reactor vessel overpressure condition would

not have occurred under certain conditions.

The inspectors reviewed the licensees overpressure analyses and discussed this issue

with regulatory assurance, operations, and engineering personnel. During the review

and discussions, the inspectors learned that both of the analyses assumed that Unit 1

and Unit 2 were operating at full thermal power. In addition, the analyses assumed that

one of the safety relief valves was inoperable. At the time this issue was identified,

neither unit was operating at full thermal power and all of the safety relief valves were

operable. Based upon this information, the inspectors concluded that this issue was not

an immediate safety concern. However, Unit 1 had operated at full thermal power levels

during the summer of 2003. In addition, one of the safety relief valves may have been

inoperable during this time (see Section 1R20 of Inspection Report 05000254/03-13;

05000265/03-13). As a result, additional information was needed to determine whether

the licensee had been in violation of their Technical Specifications and/or outside their

design and licensing basis.

At the conclusion of the inspection, the licensee was conducting reviews to determine

whether the reactor vessel was adequately protected from an overpressure condition

even though some of the main steam safety valves would not have operated within the

one percent tolerance allowed by the Technical Specifications. The licensee planned to

use the results of the review to determine whether additional actions, such as the

submittal of a Technical Specification amendment request or a Licensee Event Report,

were required. The inspectors considered this item to be unresolved pending an

inspection of the licensees review (URI 05000254/2004002-01; 05000265/2004002-01).

1R17

Permanent Plant Modifications (71111.17)

a.

Inspection Scope

During the inspection period, the inspectors reviewed the following permanent plant

modifications:

Engineering Change 342429, Add Safe Shutdown Makeup Pump Heating,

Enclosure

10

Ventilation, and Air Conditioning Room Cooler Trouble Indications and Reset

Pushbutton, Revision 0;

Engineering Change 22082, Unit 2 Reactor Recirculation Control System and Jet

Pump Instrumentation Digital Upgrade, Various Revisions;

Engineering Change 333573, Permanent Lead Shielding Around Recirculation

Risers in Unit 2 Drywell, Revision 0; and

Engineering Change 343933, Replace Unit 2 Power Operated Relief Valves with

Electromatic Relief Valves, Various Revisions.

The inspectors reviewed the design adequacy of the modifications by verifying one or

more of the following:

energy requirements were able to be supplied by supporting systems under

accident and event conditions;

replacement components were compatible with physical interfaces;

replacement component properties met functional requirements under event and

accident conditions;

replacement components were environmentally and seismically qualified;

sequence changes remained bounded by the accident analyses and loading on

support systems was acceptable;

structures, systems, and components response times were sufficient to serve

accident and event functional requirements assumed by the design analyses;

control signals were appropriate under accident and event conditions; and

affected operations procedures were revised and training needs were evaluated

in accordance with station administrative procedures.

The inspectors also verified that the post modification testing demonstrated system

operability by verifying no unintended system interactions occurred, system performance

characteristics met the design basis, and post-modification testing results met all

acceptance criteria.

b.

Findings

No finding of significance were identified.

1R19

Post Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed the post maintenance testing activities listed below during the

inspection period:

Work Order 99174178-08, Replace Portion of Unit 2 High Pressure Coolant

Injection Steam Line Drain Piping;

Work Request 135845, Troubleshoot and Repair 1/2 Emergency Diesel Generator

Fuel Oil Transfer Pump Level Switch Failure to Actuate;

Work Order 518491-01, Mechanical Maintenance Diesel Fire Pump A Annual

Inspection;

Enclosure

11

Work Order 480358-01, 250 VDC Battery Performance Test; and

Work Order 645432-01, Replace/Weld Buildup of High Pressure Discharge

Flange of 2-1001-65B Residual Heat Removal Service Water Pump Discharge

Elbow.

For each post maintenance testing activity selected, the inspectors reviewed the

Technical Specifications and Updated Final Safety Analysis Report against the

maintenance work package to determine the safety function(s) that may have been

affected by the maintenance. Following this review the inspectors verified that the post

maintenance test activity adequately tested the safety function(s) affected by the

maintenance, that acceptance criteria were consistent with licensing and design basis

information, and that the procedure was properly reviewed and approved. When

possible, the inspectors observed the post maintenance testing activity and verified that

the structure, system, or component operated as expected; test equipment used was

within its required range and accuracy; jumpers and lifted leads were appropriately

controlled; test results were accurate, complete, and valid; test equipment was removed

after testing; and any problems identified during testing were appropriately documented.

b.

Findings

No findings of significance were identified.

1R20

Refueling and Outage Activities (71111.20)

a.

Inspection Scope

The inspectors reviewed the licensees outage schedule, verified equipment alignments,

and observed control room and outage activities. The inspectors verified that the

licensee effectively conducted the shutdown, managed elements of risk pertaining to

reactivity control during and after the shutdown, and implemented decay heat removal

system procedure requirements as applicable.

The inspectors performed the following activities daily:

attended control room operator and outage management turnover meetings to

verify that the current shutdown risk status was well understood and

communicated;

performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

performed periodic walkdowns of the turbine and reactor buildings to observe

ongoing work activities; and

reviewed selected issues that the licensee entered into its corrective action

program to verify that identified problems were being entered into the program

with the appropriate characterization and significance.

Additionally, the inspectors observed the following specific activities, as appropriate:

shutdown and cooldown to a cold shutdown condition (MODE 4);

Enclosure

12

implementation of abnormal operating procedures to address any abnormal

occurrences;

initiation of the shutdown cooling mode of the residual heat removal system;

control rod withdrawals to criticality and portions of the plant power ascension;

surveillance tests throughout the duration of the outage;

troubleshooting efforts for emergent plant equipment issues;

reactor vessel disassembly and reassembly;

drywell closeout; and

reactor startup and power ascension.

b.

Findings

On February 24, Unit 2 was shutdown for a scheduled refueling outage. The scope of

the refueling outage included inspections of the steam dryer in accordance with

recommendations described in General Electric Service Information Letter 644,

Supplement 1. The inspections performed during the refueling outage identified

cracking on areas of the steam dryer that were previously modified to address the

impacts of the extended power uprate and the June 2003 Unit 2 steam dryer failure.

Due to the presence of ongoing cracking, the licensee developed a plan to attempt to

identify the mechanism that has been causing the unacceptable steam dryer loads.

Details of this plan were discussed with the NRC during conference calls on

March 8, 18, 26, and 30, 2004. Additional details were provided by the licensee to the

NRC via letter dated April 2, 2004. Within the April 2 letter, the licensee committed to

the NRC to limit operation of Quad Cities Units 1 and 2 to the maximum original licensed

power level of 2511 megawatts thermal. The units may operate for brief periods above

2511 megawatts thermal for the purposes of data gathering. However, these periods

may not exceed a total of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> for each unit.

At the conclusion of the inspection period, licensee evaluations were ongoing to justify

continuous operation of Quad Cities Units 1 and 2 at extended power uprate power

levels. The licensee planned to provide the NRC with information such as the plans for

monitoring steam dryer performance and other potentially affected components at

extended power uprate power levels, the criteria for prompt corrective action in response

to performance degradation, a description of the loads on the steam dryer, identification

of the most susceptible equipment failure locations, an evaluation of the current Unit 2

steam dryer repairs, the results of the independent review team looking at the steam

dryer and other extended power uprate issues, the results of the flow induced vibration

reviews, and the future dryer inspection plans. The NRC review of the licensees

justification for continuous operation of Quad Cities Units 1 and 2 at extended power

uprate power levels is an Unresolved Item (URI 05000254/2004002-02;

05000265/2004002-02).

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors observed surveillance testing activities and/or reviewed completed

Enclosure

13

surveillance test packages for the tests listed below:

QCOS 6500-10, Functional Test of Unit 2 Second Level Undervoltage,

Revision 13;

QCOS 6600-43, Unit 1/2 Diesel Generator Load Test, Revision 17;

QCTS 0600-05, Main Steam Isolation Valve Local Leak Rate Test, Revision 11;

QCMMS 4100-32, 1/2 A-4101 Diesel Driven Fire Pump Annual Capacity Test,

Revision 15;

QCOS 6700-02, MCC 28/29-5 Auto-Transfer Logic Operability Surveillance,

Revision 8;

QCTS 0240-07, Unit 2 250 VDC Safety Related Battery Testing, Revision 0; and

QCOS 1600-32, Drywell/Torus Closeout, Revision 10.

The inspectors verified that the structures, systems, and components tested were

capable of performing their intended safety function by comparing the surveillance

procedure or calibration acceptance criteria and results to design basis information

contained in Technical Specifications, the Updated Final Safety Analysis Report, and

licensee procedures. The inspectors verified that each test or calibration was performed

as written, the data was complete and met requirements, and the test equipment range

and accuracy were consistent with the application by observing the performance of the

activity. Following work completion, the inspectors conducted walkdowns of the

associated areas to verify that test equipment had been removed and that the system or

component was returned to its normal standby configuration. The inspectors also

reviewed multiple condition reports which were generated during the inspection to

ensure that these issues were entered into the licensees corrective action program.

b.

Findings

No findings of significance were identified.

1R23

Temporary Modifications (71111.23)

a.

Inspection Scope

The inspectors reviewed documentation for the following temporary configuration

change:

Engineering Change 345750, Use Service Water to Pressurize Residual Heat

Removal Service Water at the 2A Residual Heat Removal Heat Exchanger to

Diminish Internal Leakage, dated January 8, 2004.

The inspectors assessed the acceptability of the temporary configuration change by

comparing the 10 CFR 50.59 screening and evaluation information against the Updated

Final Safety Analysis Report and Technical Specifications. The comparison was

performed to ensure that the new configuration remained consistent with design basis

information. The inspectors performed field verifications to ensure that the modification

was installed as directed; the modification operated as expected; modification testing

adequately demonstrated continued system operability, availability, and reliability, and

Enclosure

14

that operation of the modification did not impact the operability of any interfacing

systems. The inspectors reviewed all licensee procedures impacted by the temporary

modification to ensure that the procedures were revised when required. The inspectors

also reviewed condition reports initiated during or following the temporary modification

installation to ensure that problems encountered during the installation were

appropriately resolved.

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1

Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone

a.

Inspection Scope

The inspectors discussed performance indicators (PIs) with the radiation protection staff

and reviewed data from the licensees corrective action program to determine if there

were any performance indicators for the occupational exposure cornerstone to review.

There were none. This represented one sample.

b.

Findings

No findings of significance were identified.

.2

Plant Walkdowns and Radiation Work Permit Reviews

a.

Inspection Scope

The inspectors identified three radiologically significant work areas within radiation

areas, high radiation areas, and airborne radioactivity areas in the plant. Work

packages, which included associated licensee controls and surveys of these areas,

were reviewed to determine if radiological controls including surveys, postings, and

barricades were acceptable. This represented one sample. These work areas were

walked down and surveyed (using an NRC survey meter) to verify that the prescribed

radiation work permit, procedures, and engineering controls were in place, that licensee

surveys and postings were complete and accurate, and that air samplers were properly

located. These areas included but were not limited to:

Turbine Sandblasting;

Residual Heat Removal Heat Exchanger, Leakage Repair; and

U2 Reactor Disassembly/Reassembly/Cavity Work.

This represented one sample.

Enclosure

15

The inspectors reviewed the radiation work permits and work packages used to access

these and other high radiation work areas to identify the work control instructions and

control barriers that had been specified. Technical specification high radiation area and

locked high radiation area requirements were used as standards for the necessary

barriers. Electronic dosimeter alarm set points for both integrated dose and dose rate

were evaluated for conformity with survey indications and plant policy. Workers were

interviewed to verify that they were aware of the actions required when their electronic

dosimeters noticeably malfunctioned or alarmed. This represented one sample.

The inspectors reviewed the available radiation work permits for airborne radioactivity

areas to determine if there was a potential for individual worker internal exposures of

>50 millirem committed effective dose equivalent. Barrier integrity and engineering

controls performance such as high efficiency particulate (HEPA) filtration ventilation

system operation were evaluated. Work areas having a history of, or the potential for,

airborne transuranics were evaluated to verify that the licensee had considered the

potential for transuranic isotopes and provided appropriate worker protection. This

represented one sample. The adequacy of the licensees internal dose assessment

process for internal exposures >50 millirem committed effective dose equivalent was

assessed for adequacy. This represented one sample.

b.

Findings

No findings of significance were identified.

.3

Problem Identification and Resolution

a.

Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, licensee event reports,

and special reports related to the access control program to verify that identified

problems were entered into the corrective action program for resolution. This

represented one sample. Corrective action reports related to access controls and any

available high radiation area radiological incidents (non-performance indicators identified

by the licensee in high radiation areas <1Rem/hr) were reviewed. Staff members were

interviewed and corrective action documents were reviewed to verify that follow-up

activities were being conducted in an effective and timely manner commensurate with

their importance to safety and risk based on the following:

Initial problem identification, characterization, and tracking;

Disposition of operability/reportability issues;

Evaluation of safety significance/risk and priority for resolution;

Identification of repetitive problems;

Identification of contributing causes;

Identification and implementation of effective corrective actions;

Resolution of Non-Cited Violations tracked in the corrective action system; and

Implementation/consideration of risk significant operational experience feedback.

This represented one sample.

Enclosure

16

The inspectors evaluated the licensees process for problem identification,

characterization, prioritization, and verified that problems were entered into the

corrective action program and resolved. For repetitive deficiencies and/or significant

individual deficiencies identified in the problem identification and resolution process, the

inspectors verified that the licensees self-assessment activities were capable of

identifying and addressing these deficiencies. This represented one sample.

The inspectors discussed performance indicators with the radiation protection staff and

reviewed data from the licensee's corrective action program to determine if there were

any performance indicators for the occupational exposure cornerstone to review. There

were none. This represented one sample.

b.

Findings

No findings of significance were identified.

.4

Job-In-Progress Reviews

a.

Inspection Scope

The inspectors selected three jobs being performed in radiation areas, airborne

radioactivity areas, or high radiation areas for observation of work activities that

presented the greatest radiological risk to workers. This involved work that was

estimated to result in the highest collective doses, and included diving activities in the

spent fuel pool, and other work areas where radiological gradients were present.

The inspectors reviewed radiological job requirements including radiation work permit

requirements and work procedure requirements, and attended as-low-as-is-reasonably-

achievable (ALARA) job briefings. Job performance was observed with respect to these

requirements to verify that radiological conditions in the work area were adequately

communicated to workers through pre-job briefings and postings. This represented one

sample. The inspectors also verified the adequacy of radiological controls including

required radiation, contamination, and airborne surveys for system breaches; radiation

protection job coverage which included audio and visual surveillance for remote job

coverage, and contamination controls. This represented one sample.

Work in high radiation areas having significant dose rate gradients was reviewed to

evaluate the application of dosimetry to effectively monitor exposure to personnel, and

to verify that licensee controls were adequate. These work areas involved dose rate

gradients that could be severe (diving activities and the residual heat removal heat

exchanger area) which increased the necessity of providing multiple dosimeters and/or

enhanced job controls. This represented one sample.

b.

Findings

No findings of significance were identified.

Enclosure

17

.5

High Risk Significant, High Dose Rate High Radiation Area and Very High Radiation

Area Controls

a.

Inspection Scope

The inspectors reviewed the licensees performance indicators for high risk, high dose

rate and high radiation areas, and for all very high radiation areas to verify that workers

were adequately protected from radiological overexposure. Discussions were held with

the Radiation Protection Manager concerning high dose rate/high radiation area and

very high radiation area controls and procedures, including procedural changes that had

occurred since the last inspection, in order to verify that any procedure modifications did

not substantially reduce the effectiveness and level of worker protection. This

represented one sample. During plant walkdowns, the posting and locking of entrances

to high dose rate high radiation areas, and very high radiation areas were reviewed for

adequacy. This represented one sample.

b.

Findings

No findings of significance were identified

.6

Radiation Worker Performance

a.

Inspection Scope

During job performance observations, the inspectors evaluated radiation worker

performance with respect to stated radiation protection work requirements and

evaluated whether workers were aware of the significant radiological conditions in their

workplace, the radiation work permit controls and limits in place, and that their

performance had accounted for the level of radiological hazards present. This

represented one sample.

Radiological problem reports, which found that the cause of an event resulted from

radiation worker errors, were reviewed to determine if there was an observable pattern

traceable to a similar cause, and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. These

problems, along with planned and taken corrective actions were discussed with the

Radiation Protection Manager. This represented one sample.

b.

Findings

No findings of significance were identified.

.7

Radiation Protection Technician Proficiency

a.

Inspection Scope

The inspectors observed and evaluated radiation protection technician performance with

respect to radiation protection work requirements. This was done to evaluate whether

radiation protection technicians were aware of the radiological conditions in their

Enclosure

18

workplace, the radiation work permit controls and limits were in place, and if their

performance was consistent with their training and qualifications with respect to the

radiological hazards and work activities. This represented one sample.

Radiological problem reports, which found that the cause of an event was radiation

protection technician error, were reviewed to determine if there was an observable

pattern traceable to a similar cause, and to determine if this perspective matched the

corrective action approach taken by the licensee to resolve the reported problems. This

represented one sample.

b.

Findings

No findings of significance were identified.

2OS2 As Low As Is Reasonably Achievable (ALARA) Planning And Controls (71121.02)

.1

Inspection Planning

a.

Inspection Scope

The inspectors reviewed plant collective exposure history, current exposure trends along

with ongoing and planned activities in order to assess current performance and

exposure challenges. This included determining the plants current 3-year rolling

average collective exposure in order to help establish resource allocation and to provide

a perspective of significance for any resulting inspection finding assessment. This

represented one sample.

The inspectors reviewed the outage work scheduled during the inspection period along

with associated work activity exposure estimates including the five work activities which

were likely to result in the highest personnel collective exposures. Site specific trends in

collective exposures and source-term measurements were reviewed. This represented

one sample. Procedures associated with maintaining occupational exposures ALARA,

and processes used to estimate and track work activity specific exposures were

reviewed. This represented one sample.

b.

Findings

No findings of significance were identified.

.2

Radiological Work Planning.

a.

Inspection Scope

The inspectors evaluated the licensees list of work activities ranked by estimated

exposure that were in progress and selected the three work activities of highest

exposure significance.

The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and

exposure mitigation requirements in order to verify that the licensee had established

Enclosure

19

procedures, along with engineering and work controls that were based on sound

radiation protection principles in order to achieve occupational exposures that were

ALARA. This also involved determining that the licensee had reasonably grouped the

radiological work into work activities, based on historical precedence, industry norms,

and/or special circumstances.

The inspectors compared the results achieved including dose rate reductions and

person-rem used with the intended dose established in the licensees ALARA planning

for these work activities. Reasons for inconsistencies between intended and actual work

activity doses were evaluated. The interfaces between operations, radiation protection,

maintenance, maintenance planning, scheduling and engineering groups were

evaluated to identify interface problems or missing program elements. The integration

of ALARA requirements into work procedure and RWP documents was evaluated to

verify that the licensees radiological job planning would reduce dose.

The inspectors compared the person-hour estimates, provided by maintenance planning

and other groups to the radiation protection group, with the actual work activity time

requirements in order to evaluate the accuracy of these time estimates. Shielding

requests from the radiation protection group were evaluated with respect to dose rate

reduction along with engineering shielding responses follow up. The inspectors verified

that work activity planning included consideration of the benefits of dose rate reduction

activities such as shielding provided by water filled components/piping, job scheduling,

along with shielding and scaffolding installation and removal activities. The licensees

post-job (work activity) reviews were evaluated to verify that identified problems were

entered into the licensees corrective action program.

b.

Findings

No findings of significance were identified.

.3

Verification of Dose Estimates and Exposure Tracking Systems

a.

Inspection Scope

The inspectors reviewed the assumptions and bases for the current annual collective

exposure estimate. Procedures were reviewed in order to evaluate the licensees

methodology for estimating work activity-specific exposures and the intended dose

outcome. Dose rate and man-hour estimates were evaluated for reasonable accuracy.

This represented one sample.

The licensees process for adjusting exposure estimates or re-planning work, when

unexpected changes in scope, emergent work or higher than anticipated radiation levels

were encountered, was evaluated. This included determining that adjustments to

estimated exposure (intended dose) were based on sound radiation protection and

ALARA principles and not adjusted to account for failures to control the work. The

frequency of these adjustments was reviewed to evaluate the adequacy of the original

ALARA planning process. This represented one sample.

Enclosure

20

b.

Findings

No findings of significance were identified.

.4

Job Site Inspections and As Low As Is Reasonably Achievable (ALARA) Control

a.

Inspection Scope

The inspectors selected two work activities in radiation areas, airborne radioactivity

areas, or high radiation areas for observation emphasizing work activities that presented

the greatest radiological risk to workers. Jobs that were expected to result in the

highest collective doses were observed and included diving activities in the spent fuel

pool and work in areas that involved potentially changing or deteriorating radiological

conditions. The licensees use of ALARA controls for these work activities was

evaluated using the following:

The licensees use of engineering controls to achieve dose reductions was

evaluated to verify that procedures and controls were consistent with the

licensees ALARA reviews, that sufficient shielding of radiation sources was

provided for and that the dose expended to install/remove the shielding did not

exceed the dose reduction benefits afforded by the shielding.

Job sites were observed to determine if workers were utilizing the low dose

waiting areas and were effective in maintaining their doses ALARA by moving to

the low dose waiting area when subjected to temporary work delays.

The inspectors attended work briefings and observed ongoing work activities to

determine if workers received appropriate on-the-job supervision to ensure the

ALARA requirements were met. This included verification that the first-line job

supervisor ensured that the work activity was conducted in a dose efficient

manner by minimizing work crew size, ensuring that workers were properly

trained, and that proper tools and equipment were available when the job

started.

b.

Findings

No findings of significance were identified.

.5

Source-Term Reduction and Control

a.

Inspection Scope

The inspectors reviewed licensee records to determine the historical trends and current

status of tracked plant source terms and determined that the licensee was making

allowances and had developed contingency plans for expected changes in the source

term due to changes in plant fuel performance issues or changes in plant primary

chemistry. This represented one sample.

The inspectors verified that the licensee had developed an understanding of the plant

source-term, which included knowledge of input mechanisms in order to reduce the

source term. The licensees source-term control strategy was evaluated. This included

Enclosure

21

a cobalt reduction strategy and shutdown ramping and operating chemistry plan which

was designed to minimize the source-term external to the core. Other methods used by

the licensee to control the source term, including component/system decontamination

and the use of shielding, were evaluated. This represented one sample.

The licensees process for identification of specific sources was reviewed along with

exposure reduction actions and the priorities the licensee had established for

implementation of those actions. The results that had been achieved against these

priorities since the last refueling cycle were reviewed. For the current assessment

period, source reduction evaluations were verified along with actions taken to reduce the

overall source-term compared to the previous year. This represented one sample.

b.

Findings

No findings of significance were identified.

.6

Radiation Worker Performance

a.

Inspection Scope

Radiation worker and radiation protection technician performance was observed during

work activities being performed in radiation areas, airborne radioactivity areas, and high

radiation areas that presented the greatest radiological risk to workers. The inspectors

evaluated whether workers demonstrated the ALARA philosophy in practice by being

familiar with the work activity scope and tools to be used, by utilizing ALARA low dose

waiting areas and that work activity controls were being complied with. Also, radiation

worker training and skill levels were reviewed to determine if they were sufficient relative

to the radiological hazards and the work involved. This represented one sample.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity,

.1

Reactor Safety Strategic Area

a.

Inspection Scope

The inspectors sampled the licensees performance indicator submittals for the periods

listed below. The inspectors used the performance indicator definitions and guidance

contained in Revision 2 of Nuclear Energy Institute Document 99-02, Regulatory

Assessment Performance Indicator Guideline, to verify the accuracy of the

performance indicator data. The following eight performance indicators were reviewed:

Enclosure

22

Unit 1

Unplanned Scrams per 7000 Hours;

Scrams With the Loss of Normal Heat Removal;

Reactor Coolant System Leak Rate;

System Unavailability - Residual Heat Removal System

Unit 2

Unplanned Scrams per 7000 Hours;

Scrams With the Loss of Normal Heat Removal;

Reactor Coolant System Leak Rate;

System Unavailability - Residual Heat Removal System

The inspectors reviewed selected applicable conditions and data from logs, licensee

event reports, monthly operating reports, inspection reports, licensee event reports, and

condition reports from January 2003 through December 2003 for each performance

indicator specified above to identify conditions which may have impacted the specific

performance indicator. The inspectors independently re-performed calculations where

applicable. The inspectors compared that information to the information reported for

each performance indicator to ensure that the licensee reported the data accurately.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

Routine Review of Identification and Resolution of Problems

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify that they were

being entered into the licensees corrective action system at an appropriate threshold,

that adequate attention was being given to timely corrective actions, and that adverse

trends were identified and addressed. Minor issues entered into the licensees

corrective action system as a result of inspectors observations are listed within the

individual sections of this report and are included in the list of documents reviewed

which is attached to this report.

.2

Review of Specific Problem Identification and Resolution Issues

a.

Inspection Scope

During the inspection period, the inspectors assessed the licensees ability to identify

and resolve conditions adverse to quality by direct observation of activities as part of the

baseline inspection program, performing daily reviews of condition reports, attending the

management review committee meetings which discussed previously identified

Enclosure

23

problems and proposed corrective actions, interviewing personnel, and attending

meetings on specific subjects. The inspectors selected the following three samples for

additional review:

repeated tripping of the contaminated condensate storage tank heaters;

decreasing Unit 1 reactor bottom head drain temperature; and

inadvertent isolation of the residual heat removal system while in shutdown

cooling.

b.

Issues

The inspectors determined that the licensee appropriately identified problems. However

there were several examples where individuals were presented with problems, but failed

to perform a more comprehensive review of the issue prior to taking actions. This

resulted in the inoperability of adverse weather-related equipment, the communication of

incorrect information to the operations department, and the inadvertent isolation of an

operating safety system. The inspectors noted that the licensee initiated condition

reports for each of the self-revealing issues listed above. Once the condition reports

were initiated, the licensees formal evaluation of the problem was thorough and

identified appropriate corrective actions.

Repeated Tripping of Tank Heaters

In August 1999, the licensee identified that the number of contaminated condensate

storage tank heaters in service may not have been adequate to prevent the contents of

the tank from freezing during adverse weather conditions. The inspectors reviewed this

issue since freezing of the contaminated condensate storage tanks could have led to a

situation which rendered all three high pressure injection sources unavailable or

inoperable. Through this review, the inspectors determined that eight heaters were

needed to prevent the tanks from freezing. Although previous corrective actions for the

degraded heaters had been delayed multiple times in the early 1990's, the licensee

subsequently took action to ensure that eight heaters per tank were functional. These

actions included replacing some of the heaters (see Inspection Reports 50-254/99020;

50-265/99020 and 50-254/99025; 50-265/99025).

In January 2003, the licensee discovered that the breaker for the contaminated

condensate storage tank A heating element was tripped. A followup review determined

that the feeder breaker for the motor control centers which supplied power to the

contaminated condensate storage tank heaters was overloaded. This was subsequently

corrected. In addition, the licensee worked with the heater vendor and discovered that

additional heater trips were being caused by moisture intrusion internal to the heater

circuitry and due to the age of the heaters. The vendor recommended that the licensee

implement actions to periodically energize the heaters in order to eliminate the moisture

internal to the heater circuitry. Based upon this information, engineering began working

on a modification to energize the heaters. In the interim, operations personnel

conducted routine inspections of the motor control centers when outside air

temperatures fell below 5 degrees Fahrenheit in January 2004 to ensure the heaters

remained energized.

Enclosure

24

On January 6, 2004, Quad Cities Station experienced extremely cold outside air

temperatures. Once again, some of the contaminated condensate storage tank heater

breakers began to trip. Over the next two weeks, operations personnel increased their

routine monitoring of the motor control centers to once per hour. More often than not,

the operators were identifying that the motor control center breakers supplying power to

the contaminated condensate storage tank heaters were tripped. Additional monitoring

was implemented and determined that some of the contaminated condensate storage

tank heater breakers were only remaining closed approximately 10 to 15 minutes out of

every hour. Although heater performance was worse than expected, the licensees

corrective actions focused on increased monitoring of the motor control centers and

several emergent modifications to keep the breakers from tripping rather than

performing an in-depth look at the heater circuitry in an attempt to maximize the number

of heaters that could remain operable.

Approximately one month later, operations personnel reviewed procedure

QCOP 0010-02, Required Cold Weather Routines, and discovered that operability of

the contaminated condensate storage tank heaters was based upon meeting the eight

heater continuous capability curve included in the procedure (see Condition Report

198447). Due to the frequent breaker trips, operations personnel determined that the

eight heater continuous capability curve could not be used since eight heaters were not

continuously in service. Operations personnel then tasked the engineering department

to develop a method for maintaining at least eight heaters in service within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Engineering personnel developed and implemented an additional temporary

modification which consisted of lifting a minimal number of leads to ensure that at least

eight heaters remained functional. The need for this modification was not recognized

earlier since engineering believed that the heaters would dry out and heater

performance would improve the longer the heaters remained energized.

The inspectors reviewed previous corrective actions documents, work requests,

modification information, increased monitoring information, and interviewed operations

and engineering personnel and had the following concerns:

the amount of time that elapsed before discovering the inability to meet the eight

heater continuous capability curve was excessive. For example, more than one

month was needed to make this determination even though the procedure was a

continuous use procedure which was used any time outside air temperatures

dropped below 5 degrees;

implementation of information obtained following the 1999 contaminated

condensate storage tank heater issue could have reduced the burden placed on

operations personnel during the increased monitoring inspections. In addition,

less time could have been spent designing and installing emergent modifications

which placed the plant at an increased risk during the time the tank heater

breakers were tripping. As part of the followup for the 1999 contaminated

condensate storage tank heater event engineering personnel developed

information which clearly stated the actual number of contaminated condensate

storage tank heaters that were needed under specific temperatures and wind

Enclosure

25

speeds to ensure that the contaminated condensate storage tanks would not freeze.

Although this information was available within engineering, it was not provided to the

operations department nor was it placed in the required cold weather routines

procedure.

operations personnel had not utilized the appropriate program for ensuring that

the contaminated condensate storage tank heaters remained functional. As

stated above, operations personnel were performing hourly checks of the tank

heater breakers under the increased monitoring program. The purpose of the

increased monitoring program was to outline additional items that may require

increased monitoring as deemed necessary by the shift manager or unit

supervisor. However, the inspectors determined that the operations

departments hourly checks were being performed to ensure that the freeze

protection (as described in the Updated Safety Analysis Report) remained

operable. As a result, the hourly contaminated condensate storage tank heater

breaker checks should have been considered a compensatory measure and

evaluated as part of the licensees operability determination program. The

inspectors determined that viewing the hourly checks as a compensatory

measure was not considered because the increased monitoring program

procedure was silent regarding the possibility that the increased monitoring of a

component may actually be a compensatory measure needed to ensure

continued operability. The licensee initiated Condition Report 200169 to

document the inspectors observation.

At the conclusion of the inspection period, engineering personnel had provided the

operations department with a chart which showed the specific number of contaminated

condensate storage tank heaters required under cold weather conditions. The

operations department subsequently revised the cold weather routine procedure to

include this information. Changes to the increased monitoring procedures were under

consideration. Lastly, the licensee was considering replacing multiple contaminated

condensate storage tank heaters in the future. No violations of NRC requirements were

identified during this review since the contaminated condensate storage tank heaters

were non safety-related.

Decreasing Unit 1 Reactor Vessel Bottom Head Drain Temperature

On January 8, operations personnel initiated Condition Report 194035 after identifying

that the Unit 1 reactor vessel bottom head drain temperature, as displayed on the

control room recorder, had trended down 67 degrees since December 30. The

inspectors chose this sample for additional review since an accurate indication of reactor

vessel bottom head drain temperature was needed to ensure that thermal shock did not

occur prior to starting a reactor recirculation pump. In addition, the loss of the reactor

vessel bottom head drain temperature indication would result in the licensee having to

shut down the plant if a reactor recirculation pump trip were to occur.

The following day a plant engineering supervisor performed the supervisory review for

Condition Report 194035. The supervisor noted that on December 30, the reactor

vessel bottom head drain temperature was 422 degrees Fahrenheit. The supervisor

reviewed plant drawings and identified several computer points which were also

Enclosure

26

available from the control room recorder. The supervisor performed a word search on

the computer points and identified one point which he believed depicted the reactor

vessel bottom head drain temperature. The supervisor accessed the computer point

information and found that the point was reading approximately 405 degrees Fahrenheit.

Since the computer point reading was relatively close to the bottom head drain reading

obtained on December 30, the supervisor assumed that the computer point he viewed

was indicating actual bottom head drain temperature and that the observed decrease in

bottom head drain temperature as seen on the recorder was due to a recorder problem.

Work Request 127101 was written to troubleshoot and repair the recorder. In addition,

a trend graph which used the information provided by the computer point was set up for

use by operations such that a reactor recirculation pump could be immediately restarted

if it tripped. Subsequent discussions between engineering and operations also

convinced operations personnel that the problem was with the control room recorder.

As a result, little emphasis was placed on resolving this condition.

On January 15, an instrument maintenance supervisor was reviewing Work Request 127101 and contacted the plant engineering supervisor for additional

information. Through these discussions the supervisors determined that the computer

point feeding the trend graph in the control room was for reactor vessel bottom head

temperature rather than reactor vessel bottom head drain temperature. Based upon this

information, the plant engineering supervisor concluded that if a reactor recirculation

pump had tripped, and operations personnel used the trend graph to verify that plant

conditions were acceptable for restarting the pump, the Technical Specifications would

have been inadvertently violated. Operations personnel were immediately notified of

this condition and actions were implemented to ensure that the Technical Specifications

were not violated. The engineering supervisor initiated Condition Report 195352 to

document his error. Corrective actions were in progress at the conclusion of the

inspection period. No violations of NRC requirements were identified since a reactor

recirculation pump was not started using inappropriate temperature information.

Inadvertent Isolation of Shutdown Cooling

On February 25, operations personnel performed procedure QCOP 1000-43. This

procedure provided instructions for installing two jumpers on a relay in order to prevent

the isolation of the residual heat removal system due to high reactor pressure while the

system was operating in the shutdown cooling mode. A note contained in the daily work

schedule indicated that the performance of QCOP 1000-43 could result in a loss of

shutdown cooling.

After receiving a pre-job briefing, an operator and a senior reactor operator obtained two

clip-on type jumpers for installation as directed by QCOP 1000-43. While attempting to

install the first jumper, the operator identified that the jumper would not stay attached to

the screw head located directly above relay contact #1. The operator informed the

senior reactor operator about the difficulty encountered when trying to place the jumper.

The operators discussed the situation and then identified another location on the relay

which was electrically equivalent to installing the jumper on the screw head. As the first

jumper was being installed, the operator made contact with the actual contactor and

caused a momentary power interruption. This short interruption resulted in the closure

Enclosure

27

of the inboard shutdown cooling isolation valve and a loss of the operating decay heat

removal system. The inspectors noted that decay heat removal from the reactor vessel

was restored within five minutes. No appreciable increase in reactor vessel water

temperature was identified.

Operations personnel initiated Condition Report 204095 and a prompt investigation

following this self-revealing event. The prompt investigation determined the operator

and the senior reactor operator failed to recognize that installing the jumpers in an

alternate location presented an additional risk to the plant due to the proximity to the

contacts. In addition, neither operator recognized that the additional risk should have

been evaluated prior to jumper installation. At the conclusion of the inspection period,

operations personnel had communicated this event to the remaining members of the

department. The operations department was also working with the instrument

maintenance department to determine alternate jumper installation methods and

locations which reduced the potential risk to the plant. No violations of NRC

requirements occurred since the licensee maintained the ability to operate the shutdown

cooling suction valve from the drywell if needed.

4OA3 Event Follow-up (71153)

(Closed) Licensee Event Report 50-254/03-002-01: Mode Change with Core Spray

Loop Inoperable due to Failure to Properly Fill and Vent.

During a review of the original event report, the inspectors noted that the information

contained in the Previous Occurrences section was narrowly focused. Specifically, the

licensee stated that there were no other instances of a reportable event involving the

failure to properly perform venting due to an inadequate turnover or miscommunication.

While this was true, the inspectors provided the licensee with a recently completed

common cause analysis which documented more than ten system venting events. The

inspectors also reviewed Section 5.2.5 of NUREG-1022, Event Reporting Guidelines,

with the licensee to ensure that the licensee understood that the intent of the Previous

Occurrences section of an event report was to identify any generic or recurring

problems. Based upon this information, the inspectors determined that the large

number of venting issues identified in the licensees common cause analysis should

have been included in the original event report. On February 19, 2004, the licensee

revised the original event report to include additional system venting events at Quad

Cities in the Previous Occurrences section of the report. The inspectors reviewed the

new information and had no additional concerns.

(Closed) Licensee Event Report 50-254/03-003-00: Failure of Reactor Main Steam

Relief Valve Actuator Following Failure of the Pilot Valve Vent Line.

Introduction: The inspectors identified a Green finding and Non-Cited Violation due to

the Unit 1, 1-0203-3B electromatic relief valve being found in an inoperable condition.

Enclosure

28

Description: On November 12, 2003, Unit 1 was shut down to repair the steam dryer.

While performing drywell local area surveys, radiation protection personnel identified

that the 3B electromatic relief valve pilot valve vent line was broken off at the pilot valve

chamber assembly. Condition Report 186700 was initiated and Work Order 638286

was written to facilitate repairs.

On November 17, 2003, electrical maintenance technicians discovered internal damage

to the electromatic relief valve actuator. The left side spring supporting the solenoid

plunger was protruding through the brass bushing and one of two internal limit switches

was missing from the limit switch arm. Based upon this information, the 3B electromatic

relief valve solenoid actuator was removed and taken to the electrical maintenance shop

for testing. The technicians determined that the solenoid actuator failed to operate in its

current condition and thereby would not have opened the 3B electromatic relief valve

when required. The licensee suspected that the 3B electromatic relief valve pilot

solenoid actuator components were damaged due to increasing vibrations that occurred

while the plant operated at power with the pilot vent line severed from the pilot valve

chamber assembly.

The root cause of the 3B electromatic relief valve pilot valve vent line break was

determined to be a lack of standard procedural instruction to identify, evaluate, and

resolve issues concerning the cold spring forces on the small-bore lines during the 3B

electromatic relief valve installation. The licensee concluded that the 3B electromatic

relief valve pilot vent line failure resulted from fatigue cracking of the vent line under

operating conditions. Analysis of the failed section of pipe indicated that the 1-inch

carbon steel pilot vent line failed by fatigue due to a synergistic combination of stresses.

These included residual installation stresses, bending, and operational vibration

stresses concentrated at the toe of the vent line weld. This weld location was

susceptible as a stress-riser due to the cross sectional change from the 3B electromatic

relief valve body to the 1-inch pipe, a 20-mil deep mechanical indentation, and weld

voids observed within this indentation. The cumulative affect of these issues led to the

pipe failure when added to the pipe stress induced by the cold spring found in the pilot

vent line.

Analysis: The inspectors determined that the failure to implement adequate procedural

guidance to prevent cold spring stresses from degrading safety-related components to

the point of inoperability beyond the Technical Specification limits was more than minor

because it impacted the equipment performance and protection against external factors

performance attributes of the mitigating systems cornerstone. In addition, this finding

impacted the cornerstone objective of ensuring the availability, reliability, and capability

of a system that responds to initiating events to prevent undesirable consequences

since the electromatic relief valve was part of the automatic depressurization system.

The inspectors determined that this finding should be evaluated in accordance with

Inspection Manual Chapter 0609, Significance Determination Process, (SDP) because

the finding was associated with the operability, availability, reliability, and function of the

Automatic Depressurization System function of the Low Pressure Coolant Injection

System. The inspectors consulted the Significance Determination Process Phase 1

Enclosure

29

worksheet and determined that a Phase 2 evaluation was required based upon the

finding representing an actual loss of safety function of a single train for greater than its

Technical Specification Allowed Outage Time.

The inspectors used the Risk-Informed Inspection Notebook for Quad Cities Nuclear

Power Station, Units 1 and 2, Revision 1, dated May 2, 2002, to complete the Phase 2

evaluation. The inspectors determined that the exposure time was greater than 30 days

since the electromatic relief valve was determined to have been inoperable from

approximately July 23 to November 11, 2003. For each Significance Determination

Process worksheet completed, the inspectors assumed that all mitigating systems

equipment was available except for the specific electromatic relief valve. The inspectors

allowed credit for manual operator action to open additional electromatic relief valves if

required during the accident condition. Using these assumptions, the inspectors

evaluated nine core damage sequences. Worksheet results ranged from 7 to 12 points.

The most dominant core damage sequence involved a medium Loss of Coolant

Accident followed by a Transient without Power Conversion System and Loss Of Off-site

Power. Based on the counting rule, the overall increase in risk was determined to be 7,

therefore, the regional Senior Reactor Analyst evaluated the finding for both large early

release frequency (LERF) and external event significance.

Utilizing Inspection Manual Chapter 0609, Appendix H, Containment Integrity SDP,

draft Appendix H, and NUREG 1765, Basis Document for LERF SDP, the Senior

Reactor Analyst concluded external events were not a major contributor to the overall

risk significance to the finding. Therefore, this finding was of very low safety

significance (Green) based on credit given to operators mitigating capability for taking

manual action for depressurization and the fact that other mitigating systems were

available.

Enforcement: Technical Specification 3.4.3.A requires that with one relief valve

inoperable, restore the valve to operable status within 14 days or be in mode 3 within

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. In addition, Technical Specification 3.5.1.G

requires that with one automatic depressurization system valve inoperable, restore the

valve to operable status within 14 days or be in mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and reduce

reactor dome pressure to 150 psig or below within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Contrary to the above, the

licensee discovered on November 15, 2003, that automatic depressurization system

valve 1-0203-3B was inoperable when required to be operable from July 23 until

November 11, 2003. This violation is being treated as a Non-Cited Violation, consistent

with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000254/2004002-03). This

violation is in the licensees corrective action program as Condition Report 186700.

Corrective actions for this event included repairing the electromatic relief valve and

inspecting the remaining valves to ensure that they remained operable.

4OA5 Other Activities

(Closed) Temporary Instruction 2515/154: Spent Fuel Material Control and Accounting

at Nuclear Power Plants. The inspectors completed Phase I and Phase II of the subject

temporary instruction and provided the appropriate documentation to NRC management

as required by the temporary instruction.

Enclosure

30

(Closed) Unresolved Item 50-254/01-08-02: Calculations of Air in the High Pressure

Coolant Injection and Reactor Core Isolation Cooling Lines Dont Appear to Support

Operability. After this item was opened, Dresden Station experienced a significant water

hammer within their high pressure coolant injection system. The root cause of this

event and items which contributed to this event were reviewed by the Quad Cities

Station engineering staff to ensure that Quad Cities was not susceptible to the same

type of event. Calculations were also reviewed to ensure adequate margin was

available to minimize a potential water hammer event. Corrective actions were

implemented as needed following this review. The Quad Cities engineering staff also

completed a common cause evaluation of approximately ten system venting issues.

The licensee determined that several of the venting issues were created due to

procedural inadequacies. The inspectors reviewed the licensees common cause

evaluation for completeness, accuracy, and implementation of the associated corrective

actions. No problems were identified.

(Closed) Unresolved Item 50-254/02-08-02; 50-265/02-08-02: Missed Inspections of the

Control Rod Drive Housing Welds. This issue was reviewed by the Office of Nuclear

Reactor Regulation. The NRC staff concluded that boiling water reactors that have not

updated to the 1995 Edition of the Code, and apply the exemption of IWB-1220 do not

have to inspect the control rod drive housings. Quad Cities is an ASME 1989 Code

Edition plant. To demonstrate the makeup capability of the reactor core isolation cooling

and safe shutdown makeup pump systems, the licensee performed Design Analysis

No. QDC-0200-M-1279. The analysis found that the makeup capability of 109 lb/sec (800 gpm) of the reactor core isolation cooling and safe shutdown makeup pump

systems is greater than the potential leakage of 75 lb/sec due to a weld failure in the

control rod drive housing. For Quad Cities, the control rod drive housings would be

exempt from surface and volumetric examinations per ASME,Section XI, IWB-1220(a).

(Closed) Unresolved Item 50-254/03-013-05: Unexpected Damage to the Electromatic

Relief Valves due to Vibration. This issue was discussed in the closure of Licensee

Event Report 05000254/2003003-00, Failure of Reactor Main Steam Relief Actuator

Following Failure of the Pilot Valve Vent Line. (See Section 4OA3 of this report for

additional details).

4OA6 Meetings

.1

Exit Meeting

The inspectors presented the inspection results to Mr. T. Tulon and other members of

licensee management at the conclusion of the inspection on April 6, 2004. The

inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

Enclosure

31

.2

Interim Exit Meetings

Interim exits were conducted for:

Inservice inspection with Mr. T. Tulon on March 5, 2004.

Access control to radiologically significant areas and the ALARA planning and

controls programs with Mr. T. Tulon on March 5, 2004.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Tulon, Site Vice President

R. Gideon, Plant Manager

B. Swenson, Plant Manager (former)

R. Armitage, Training Manager

D. Barker, Radiation Protection Manager

W. Beck, Regulatory Assurance Manager

T. Bell, Acting Engineering Manager

G. Boerschig, Work Control Manager

T. Hanley, Maintenance Manager

D. Hieggelke, Nuclear Oversight Manager

K. Leech, Security Manager

R. May, NDE Level III

K. Moser, Chemistry/Environ/Radwaste Manager

K. Ohr, ALARA Supervisor

M. Perito, Operations Manager

T. Wojcik, Engineering Programs Supervisor

Nuclear Regulatory Commission

M. Ring, Division of Reactor Projects - Branch 1

L. Rossbach, Office of Nuclear Reactor Regulation

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000254/2004002-01

URI

Ability of Main Steam Valves to Meet Technical

05000265/2004002-01

Specification Surveillance Requirement 3.4.3.1.

(Section 1R15)05000254/2004002-02

URI

Extended Power Uprate Power Levels (Section 1R20)05000265/2004002-02

05000254/2004002-03

NCV

Automatic Depressurization System Valve 1-0203-3B was

Inoperable When Required to be Operable (Section 4OA3)

Closed

05000254/2004002-03

NCV

Automatic Depressurization System Valve 1-0203-3B was

Inoperable When Required to be Operable

Attachment

2

05000254/2003013-05

URI

Unexpected Damage to the Electromatic Relief Valves due

to Vibration

05000254/2003002-01

LER

Mode Change with Core Spray Loop Inoperable due to

Failure to Properly Fill and Vent

05000254/2003003-00

LER

Failure of Reactor Main Steam Relief Valve Actuator

Following Failure of the Pilot Valve Vent Line

05000254/2001008-02

URI

Calculations of Air in the High Pressure Coolant Injection

and Reactor Core Isolation Cooling Lines Dont Appear to

Support Operability

05000254/2002008-02

URI

Missed Inspections of the Control Rod Drive Housing 05000265/2002008-02

Welds

Attachment

3

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01

Adverse Weather

QCOS 0005-05; Increased Monitoring Surveillance; Revision 8

Updated Final Safety Analysis Report

Calculation QDC-3300-M-0872; CCST Time-Temperature Response Under Various

Scenarios; Revision 0A

QCOP 0010-02; Required Cold Weather Routines; Revision 14

Temporary Configuration Change Permit 346527; Install Relay Block to Maintain CCST

Heaters Functionality; dated January 7, 2004

Temporary Configuration Change Permit 347103; Document Leads Lifted for CCST

Heaters - Declared Emergent; dated February 4, 2004

Condition Report 198447; CCST Tank Heater Breakers Frequently Tripping; dated

January 30, 2004

Condition Report 197261; Emergent Modification on CCST/CST Heater Pushbutton

Locks; dated January 23, 2004

Condition Report 193621; CCST Heater Reliability; dated January 6, 2004

Condition Report 198072; Recurring Heating System Problems; dated January 28, 2004

Condition Report 200169; CCST Heaters - Use of Increased Monitoring as a

Compensatory Action; dated February 6, 2004

1R04

Equipment Alignment

QOM 1-2300-01; Unit 1 HPCI Valve Checklist; Revision 8

QOM 1-2300-02; HPCI System Fuse and Breaker Checklist; Revision 4

QCOS 2300-10; HPCI Monthly Valve Position Verification; Revision 7

QCAN 901(2)-3 B-16; Core Spray Discharge Header Hi/Lo Pressure; Revision 9

Attachment

4

QCOS 0010-7; Equipment External Leakage Test; Revision 2

QCOP 1400-01; Core Spray System Preparation for Standby Operation; Revision 15

QCOP 1000-44; Unit 2 Alternate Decay Heat Removal; Revision 12

Piping and Instrumentation Diagram M-78; Diagram of Core Spray Piping; dated

July 27, 1999

QOM 2-1400-08; Core Spray System Fuse and Breaker Checklist; Revision 4

QOM 2-1400-09; Unit 2 Core Spray Valve Checklist; Revision 3

QOM 2-1400-10; 2B Core Spray Valve Checklist; Revision 3

Bearing Oil Analyses for 2B Core Spray Pump; dated December 8, 2003

Bearing Oil Analyses for 2A Core Spray Pump; dated January 21, 2004

Condition Report 205717; Inadequate Thread Engagement on 1-1402-28B Inlet Flange

Stud; dated March 3, 2004

Condition Report 205862; Wrong Oil in the 2A Core Spray Motor Upper and Lower

Reservoir; dated March 3, 2004

Condition Report 205892; Wrong Oil in the 2B Core Spray Motor Upper and Lower

Reservoir; dated March 3, 2004

Condition Report 205902; Incorrect Oil Labels on Upper and Lower Bearing Reservoirs

1B Core Spray; dated March 3, 2004

Condition Report 205908; No Oil Label on Upper or Lower Bearing Reservoirs 2B Core

Spray Motor; dated March 3, 2004

Condition Report 205910; No Oil Label on Upper Oil Reservoir for 2A Core Spray Motor;

dated March 3, 2004

Piping and Instrumentation Diagram 1900-01; Fuel Pool Cooling System; Revision 3

QCOP 3700-02; RBCCW System Startup and Operation; Revision 17

QCOP 1900-20; Using Fuel Pool Cooling System to Clean Up Reactor

Cavity/Dryer-Separator Water; Revision 8

QCOP 1900-24; Unit 2 Fuel Pool Cooling System Startup and Shutdown; Revision 5

QOM 2-1900-01; U2 Fuel Pool Cooling Valve Checklist; Revision 5

Attachment

5

QOM 2-3700-01; U2 RBCCW Valve Checklist; Revision 6

1R05

Fire Protection

OP-AA-201-005; Fire Brigade Qualification; Revision 2

OP-AA-201-003; Fire Drill Performance; Revision 6

QCMMS 4100-01; Fire Extinguisher and Hose Reel Inspection; Revision 18

OP-AA-201-001; Fire Marshall Tours; Revision 2

QCOA 0010-12; Fire/Explosion; Revision 24

Scenario for First Quarter 2004 Fire Drill

Quad Cities Units 1 and 2 Pre-Fire Plans

Quad Cities Units 1 and 2 Fire Hazards Analysis

Condition Report 198002; SCBA Respirator Failed During Fire Drill; dated January 28,

2004

Condition Report 204252; Weakness of First Quarter Fire Brigade Drills; dated

February 19, 2004

EP-AA-1006; Quad Cities Units 1 and 2 Emergency Action Levels

1R07

Heat Sink

Updated Final Safety Analysis Report

Technical Specifications

QCOS 1000-29; RHR Heat Exchanger Thermal Performance Test; Revision 10

TIC-856; Allow IMD to Install Fluke at an Alternate Location for Flow Transmitter; dated

February 9, 2004

1R08

Inservice Inspection

GE-PDI-UT-1; PDI Generic Procedure for the Ultrasonic Examination of Ferritic Piping

Welds; dated December 9, 2003

AR #00132435; Jet Pump No. 2 and No. 7 AD-3b Cracks

Attachment

6

1R13

Risk Assessment and Emergent Work

Daily Work Schedule; dated January 25-31, February 9-14, February 16-21, February

23-28, and March 8-13, 2004

Work Week Safety Profile for Weeks Ending January 31, February 14, February 21,

February 28, and March 8, 2004

Exelon Risk Analysts Review Notes for Weeks of January 26, February 9, February 16,

February 23, and March 8.

WC-AA-104; Review and Screening for Production Risk; Revision 7

WC-AA-101; On-Line Work Control Process; Revision 8

1R14

Non-Routine Evolutions

Unit 2 Control Room Logs; dated February 2 and March 30 through 31, 2004

QCGP 3-1; Reactor Power Operations; Revision 38

QCOA 3500-01; Feedwater Temperature Reduction with Main Turbine On Line;

Revision 21

QCOP 3500-05; Removing Low Pressure Feedwater Heaters From Service; Revision 8

QCOP 3500-03; Removing High Pressure Heaters From Service; Revision 10

QCOS 5600-10; Unit 2 Weekly Turbine Generator Tests; Revision 2

QCGP 2-3; Reactor Scram; Revision 49

QCGP 2-5; Post Scram Review; Revision 18

QGA 100; RPV Control; Revision 7

Condition Report 124187; 1D1 Heater Feedwater Side Relief Valve Blowing by Seat;

dated September 23, 2003

Condition Report 198453; Unit 2 Feedwater Heater Condensate Side Relief Valve

Leaking; dated January 25, 2004

Condition Report 198863; Emergency Load Drop due to Relief Valve 2-3621 Lifting;

dated February 2, 2004

Condition Report 199065; Lessons Learned from 2D1 Heater Response; dated

February 2, 2004

Attachment

7

Unplanned Spread of Contamination due to 2D1 Heater Valve; dated February 2, 2004

Turbine Building Floor Drain Sump and Equipment Drain Sump Information; dated

February 2, 2004

1R15

Operability Evaluations

Operability Evaluation 179235-08; Reactor Pressure Vessel Pressure and Temperature

Limits; Revisions 0 and 1

Condition Report 179235; Potentially Non-Conservative Pressure Temperature Curves;

dated October 3, 2003

Letter RS-03-113 from Patrick Simpson, Exelon Nuclear to USNRC Document Control

Desk; Reactor Coolant System Pressure and Temperature Limits; dated June 6, 2003

Condition Report 100198; 125 Volt DC Ground on 3E Power Operated Relief Valve;

dated March 20, 2002

Condition Report 99640; Level 3 Ground Unit 2 125 Volt Battery System; dated

March 17, 2002

Condition Report 99577; Unit 2 125 Volt Battery Ground; dated March 16, 2002

Operability Evaluation 191530-08; 125 Volt DC Grounds on Two Power Operated Relief

Valves; Revisions 0 and 1

Engineering Change Evaluation 343209; Engineering to Determine Correct Method to

Adjust the Power Operated Relief Valve Limits; dated June 6, 2003

Engineering Change 340635; Lift Leads at 2-2202-32 Panel to Alleviate a 125 Volt DC

Ground on the 2-0203-3E Annunciator Circuit; dated January 17, 2003

Engineering Change 346384; Lift Leads in 2-0203-3E Power Operated Relief Valve

Indicating Circuit to Remove 125 Volt DC Ground; dated December 19, 2003

Engineering Change 346449; Lift Leads in 2-0203-3B Power Operated Relief Valve

Indicating Circuit to Removed 125 Volt DC Ground; dated December 26, 2003

Operability Evaluation 148103; Moore Industries SCT Signal Converter/Isolator;

Revision 2

Dresden Operability Evaluation 03-005; Moore Industries SCT Signal Converter/Isolator;

Revision 0

Engineering Evaluation 347865; Assess Past Operability of Unit 2 Core Spray Pumps

With Wrong Oil; dated March 12, 2004

Attachment

8

Email from Bruce Jarnot, Exxon Mobil Corporation to Gerald Frizzell, Exelon

Corporation; dated June 28, 2001

GENE Letter from W. J. Roit, GENE Electrical Services, to Larry King, Exelon

Corporation; Subject: Dresden/Quad Cities Core Spray and Low Pressure Coolant

Injection Motor and Pump Mechanical Seal Elevated Cooling Water Temperature

Evaluation; dated March 16, 2001

GENE Letter DRF A61-0053 from W. J. Roit, GENE Electrical Services, to Larry King,

Exelon Corporation; Subject: Dresden/Quad Cities Core Spray and Low Pressure

Coolant Injection Motor and Pump Mechanical Seal Elevated Cooling Water

Temperature Evaluation; dated May 2, 2001

GENE Project Task Report; Dresden and Quad Cities Extended Power Uprate

Containment Systems Response Report; dated December 2000

1R17

Permanent Plant Modifications

Engineering Change 22082; Unit 2 Reactor Recirculation Control and Jet Pump

Instrumentation Upgrade

TIC-0864; Unit 2 Reactor Recirculation Control System and Jet Pump Instrumentation

Digital Upgrade; Revision 0

Digital Recirc Module for the Licensed Operator Initial Training Program; Reactor

Recirculation Control System; Revision 0

Condition Report 203524; Engineering Change 22082 had Miscellaneous Deficiencies

Requiring Revision; dated February 3, 2004

Engineering Change 342429; Add Safe Shutdown Makeup Pump Heating, Ventilation,

and Air Conditioning Room Cooler Trouble Indications and Reset Pushbutton;

Revision 0

Drawing Changes Associated with Engineering Change 342429

Condition Report 191445; Safe Shutdown Makeup Pump Room Cooler Modification

Test Revision; dated December 17, 2003

Engineering Change 333573; Permanent Lead Shielding Around Recirculation Risers in

Unit 2 Drywell; Revision 0

Engineering Change 343933; Replace Unit 2 PORVs with ERVs; Revision 0

Updated Final Safety Analysis Report

Technical Specifications

Attachment

9

1R19

Post Maintenance Testing

Updated Final Safety Analysis Report

Condition Report 207589; Fuel Oil Day Tank Alarm Received During QCOS 6600-43;

dated March 12, 2004

QCOS 6600-03; Diesel Fuel Oil Transfer Pump Monthly Operability; Revision 16

Prompt Investigation for Condition Report 206673; Secondary Containment Breach

Following High Pressure Coolant Injection Steam Line Drain Replacement; dated

March 8, 2004

Plant Barrier Impairment Permit 2004-42; dated March 5, 2004

QOP 0020-01; Opening a Penetration in Secondary Containment; dated March 6, 2004

Condition Report 206673; Secondary Containment Breach Following High Pressure

Coolant Injection Steam Line Drain Replacement; dated March 6, 2004

Condition Report 206294; Plant Barrier Impairment not Initiated for Core Boring into

Secondary Containment; dated March 5, 2004

QCMMS 4100-31; Annual Cummins Diesel Fire Pump Engine Inspection; Revision 8

Condition Report 200622; Nuclear Oversight Identified QCMMS 4100-32

Enhancements; dated February 9, 2004

Work Order 542317-01; Mechanical Maintenance Diesel Fire Pump A Capacity Test;

dated February 9, 2004

Condition Report 200717; 1/2 A Diesel Fire Pump Degrading Trend; dated February 10,

2004

QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 17

QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 17

PMED-891377-01; Development of a Duty Cycle Based on a More Conservative

Application of Coincident Starting Currents for the 250 VDC Battery System; Revision 0

1R20

Refueling and Outage

GENE Services Information Letter 664, Supplement 1; BWR Steam Dryer Integrity;

dated September 5, 2003

Q2R17 Shutdown Safety Overview; no date available

Attachment

10

Q2R17 Level 1 Schedule; dated February 11, 2004

Quad Cities Unit 2 Steam Dryer Inspection Handout; dated March 8, 2004

Quad Cities Unit 2 Steam Dryer Repairs Handout; dated March 24, 2004

Quad Cities Unit 2 Shutdown Safety Profile; various dates

Q2R17 Key Systems Used for Shutdown Safety; various dates

General Electric Field Deviation Disposition Request EE2-0537; dated March 2, 2004

General Electric Field Deviation Disposition Request EE2-0538; dated March 3, 2004

Indication Notification Report Q2R17-04-01; Dryer Internal Lower Strut Indication; dated

February 26, 2004

Indication Notification Report Q2R17-04-02, Revision 1; Dryer Internal Upper Support

Indications; dated February 28, 2004

Indication Notification Report Q2R17-04-03; Dryer Drain Channel and Skirt Indications;

February 27, 2004

Indication Notification Report Q2R17-04-04, Revision 3; Dryer Internal Horizontal Weld

Indications; dated March 2, 2004

Indication Notification Report Q2R17-04-05; Dryer Internal Vertical Weld Indication;

dated February 28, 2004

Indication Notification Report Q2R17-04-06; Revision 3; Dryer Guide Channel Indication;

dated March 3, 2004

Indication Notification Report Q2R17-04-07; Dryer Drain Channel Indications DC-A-180;

dated February 28, 2004

Indication Notification Report Q2R17-04-08; Steam Dryer Exterior End Plate Indications;

dated February 29, 2004

Indication Notification Report Q2R17-04-09; Steam Dryer Exterior Tie Bar Indications;

dated March 1, 2004

Indication Notification Report Q2R17-04-10; Steam Dryer Exterior Hold Down

Assemblies; dated March 2, 2004

Indication Notification Report Q2R17-04-11; Steam Dryer Outer Hood Gussets; dated

March 2, 2004

Attachment

11

Indication Notification Report Q2R17-04-12; Steam Dryer Exterior Hood Plate

Indications; dated March 3, 2004

Indication Notification Report Q2R17-04-13; Guide Rods; dated March 7, 2004

Indication Notification Report Q2R17-04-15; Jet Pump Wedges; dated March 8, 2004

Indication Notification Report Q2R17-04-16, Revision 1; Feedwater Sparger Brackets;

dated March 9, 2004

Indication Notification Report Q2R17-04-17; Top Guide Rim Weld 11; dated March 9,

2004

Indication Notification Report Q2R17-04-18; Perforated Plate 1, 2, 3, and 21 Weld

Indications; dated March 21, 2004

Indication Notification Report Q2R17-04-19; Horizontal Plate 17, 16, and 19 Weld

Indications; dated March 22, 2004

Indication Notification Report Q2R17-04-20; Perforated (Horizontal) Plate 06 and 07

Weld Indications; dated March 22, 2004

1R22

Surveillance Testing

Updated Final Safety Analysis Report

Technical Specifications

Work Order 648518-01; Diesel Generator Load Test

Work Order 600010-01; Diesel Generator Timed Start

NUREG-1022; Event Reporting Guidelines 10 CFR 50.72 and 50.73; Revision 2

Condition Report 199755; Bus 24-1 Degraded Voltage Relays Found Out of Tolerance;

dated February 5, 2004

Condition Report 199880; Nuclear Oversight Identified Peer Check Used in Lieu of

Concurrent Verification; dated February 5, 2004

Drawing 4E-2334; Relaying and Metering Diagram 4160 Volt Switchgear Buses 23-1

and 24-1; Revision AD

Drawing 4E-2346; Schematic Drawing 4160 Volt Bus 24-1 Standby Diesel 2 Feed and

24-1 Tie Breaker Sheet 1; Revision AM

Drawing 4E-2346; Schematic Drawing 4160 Volt Bus 24-1 Standby Diesel 2 Feed and

24-1 Tie Breaker Sheet 2; Revision AN

Attachment

12

Q2R17 Main Steam Isolation Valve Local Leak Rate Test Results and Recovery Plan

QCTP 0130-01; Leak Rate Testing Program; Revision 17

QCMMS 4100-31; Annual Cummins Diesel Fire Pump Engine Inspection; Revision 8

Condition Report 200622; Nuclear Oversight Identified QCMMS 4100-32

Enhancements; dated February 9, 2004

Work Order 542317-01; Mechanical Maintenance Diesel Fire Pump A Capacity Test;

dated February 9, 2004

Condition Report 200717; 1/2 A Diesel Fire Pump Degrading Trend; dated February 10,

2004

QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 17

Condition Report 196912; Auto Transfer of MCC 28/29-5 Time Out of Tolerance; dated

January 22, 2004

Condition Report 131936; Missing Bellville Washer in 1-0203-2C MSIV; dated

November 16, 2002

Condition Report 203885; As Found Local Leak Rate Test Main Steam Isolation Valve

Max Pathway Greater than 46 scfm; dated February 24, 2004

QCTS 0210-04; Setup and Use of the BCT-2000 Battery/Charger Test Computer;

Revision 3

QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 17

PMED-891377-01; Development of a Duty Cycle Based on a More Conservative

Application of Coincident Starting Currents for the 250 VDC Battery System; Revision 0

Work Order 481760; Drywell Closeout; dated March 27, 2004

1R23

Temporary Modifications

Engineering Change 345750; Use Service Water to Pressurize Residual Heat Removal

Service Water at 2A Residual Heat Removal Heat Exchanger to Minimize Internal

Leakage; Revision 1

Drawing Changes Associated with Engineering Change 345750

Updated Final Safety Analysis Report

Technical Specifications

Attachment

13

CC-AA-112; Temporary Configuration Changes; Revision 7

2OS1 Access Control to Radiologically Significant Areas

2OS2 ALARA Planning And Controls

CR 204161; Venture Carpenter Exited The RCA Wearing A Skull Cap; February 25,

2004

CR 204085; Found Dosimeter Alarming In U2 RCIC/2B Core Spray Room; February 25,

2004

AR 185378185378 Recommendations For WBC Program Improvements; November 7, 2003

AR 186161186161 Scorecard Trend Of Dosimetry Issues; November 12, 2003

AR 186509186509 Unplanned Spread Of Contamination; November 14, 2003

AR 186575186575 Individual Arrived At QC With Contaminated Shoes; November 9, 2003

AR 187056187056 Unplanned Spread Of Contamination (U2 Sample Panel); November 17,

2003

AR 187067187067 Unplanned Spread Of Contamination (U1 EHC Skid); November 16, 2003

AR 187439187439 Unable To Release LHRA Due To Inadequate Flush; November 20, 2003

AR 187825187825 Contaminated Water Draining Onto The MSIV Room Floor; November 21,

2003

AR 188443188443 Heavy Items Hanging From Unit 1 SFP Hand Rail; November 29, 2003

AR 188600188600 INPO Assist Visit Identified Weaknesses In Exposure Control; October 31,

2003

AR 188602188602 INPO Assist Visit Identified Weaknesses In Contamination Control;

October 31, 2003

AR 189809189809 Individual E.D. Alarm Investigation; December 6, 2003

AR 191806191806 Higher Than Expected Dose Rates On The 1-1904-46A Valve;

December 16, 2003

CR 204657; Q2R17-PCE Hooking Up Decon Equipment DW Basement; February 26,

2004

CR 204527; Worker Lost Electronic Dosimeter; February 27, 2004

AR 192402192402 Emergent Dose Cleaning RW Basement; December 17, 2003

Attachment

14

AR 197351197351 Radiological Postings in The RCA Dont Match RWP Instructions;

January 1, 2004

AR 197647197647 Workers Entered HRA Without HRA Brief; January 26, 2004

AR 198903198903 Unplanned Spread Of Contamination Due To 2D1 Heater Valve;

February 2, 2004

AR 202191202191 Unplanned Spread Of Contamination Due To Leaching; February 14, 2004

LS-AA-126-1005; CHECK-IN Self Assessment Report: ALARA Planning and Controls;

February 20, 2004

NOSPA-QC-03-2Q; Continuous Assessment Report; July 30, 2003

NOSPA-QC-03-4Q; Continuous Assessment Report; January 23, 2004

NOSPA-QC-03-3Q; Continuous Assessment Report; October 28, 2003

NOSA-QDC-03-06; NOS HP/RP Audit Exit Report; May 21, 2003

RWP 10003160; ALARA/RP Brief: Q2R17 Sandblasting (Turbine); February 26, 2004

RWP 10003560; ALARA Plan: (U2 DW) Replace Four PORVs With ERVs; February 23,

2004

RWP 10003074; ALARA Plan: (U2 DW) Control Rod Drives: Remove/Replace;

February 18, 2004

RWP 10003566; ALARA Plan: (U2 DW) Weld Overlays; February 19, 2004

RWP 10003100; ALARA Plan: (U2 DW) 21-0220-57A RFW Valve Repair; February 18,

2004

RWP 10003535; ALARA Plan: 2A RHR Heat Exchanger: Repair Internal Leakage;

February 18, 2004

RWP 10003171; ALARA Plan: U2 RX Disassembly/Reassembly/Cavity Work/Wall

Cleaning; February 18, 2004

RWP 10003159; U2 Main Turbine Overhaul/PM; February 23, 2004

RWP 10003830; Ultrasonic Fuel Cleaning; Revision 1

RP-AA-401; Operational ALARA Planning and Control; Revision 2

RP-AA-222; Methods For Estimating Internal Exposure From In Vivo and In Vitro

Bioassay Data; Revision 1

Attachment

15

10003559; Work In Progress Review: U2 DW Permanent Shielding; March 4, 2004

10003142; Work In Progress Review: Outboard MSIV: Internal Valve Repairs; March 3,

2004

10003181; Work In Progress Review: U2 Rx Steam Dryer: Tie-Bar Repair (Divers);

February 29, 2004

10003171; Work In Progress Review: U2 Rx Disassembly/Reassembly; February 27,

2004

10003832; Work In Progress Review: 2-1203-C RWCU HX: Remove Furminite

Clamp/Repair; March 2, 2004

10003830; Work In Progress Review: BWR Fuel Cleaning: Ultrasonic Fuel Cleaning

Pilot Campaign; January 28 and 30, 2004

LS-AA-104-1001; Ultrasonic Cleaning of GE 14 Bundles; Revision 1

CR 198111; Fuel Bundle FME and Spacer Changes After Ultrasonic Cleaning;

January 29, 2004

BWR Fuel Cleaning Status; September 8, 2003

BRAC Data Unit 2; Three Year Rolling Average; March 4, 2004

Unit 2, A and B Recirc Loops; BRAC Point Dose Rates; March 3, 2004

Unit 2 Drywell Surveys; February 24 and March 1, 2004

4OA1 Performance Indicator Verification

Control Room Logs; dated January through December 2003

LS-AA-2010; Monthly Performance Indicator Data Elements for Unplanned Scrams per

7000 Critical Hours; Revision 3

LS-AA-2020; Monthly Performance Indicator Data Elements for Unplanned Scrams with

Loss of Normal Heat Removal; Revision 3

LS-AA-2070; Monthly Performance Indicator Data Elements for Safety System

Unavailability - Residual Heat Removal Systems; Revision 3

LS-AA-2100; Monthly Performance Indicator Data Elements for Reactor Coolant System

Leakage; Revision 4

Attachment

16

4OA3 Event Follow-up

Condition Report 186979; 3B ERV Actuator Found Damaged; dated November 17, 2003

Condition Report 187787; 3C ERV Showing Excessive Wear; dated November 22, 2003

Condition Report 187788; 3D ERV Shows Excessive Wear; dated November 22, 2003

Condition Report 187789; 3E ERV Shows Excessive Wear; dated November 22, 2003

Condition Report 188202; Documentation Results of Extent of Condition for ERV

Vibration; dated November 25, 2003

Condition Report 188204; Dresser ERV Torque Specifications Not Included in

Procedures; dated November 25, 2003

4OA5 Other Activities

Temporary Instruction 2515/154; Spent Fuel Material Control and Accounting at Nuclear

Power Plants; dated November 26, 2003

Quad Cities Station Annual Physical Inventory; dated July 14, 2003

Special Nuclear Material Monthly Report; dated January 1, 2004

NF-AA-310; Move Cover Sheet for Inspection of Leaker Assembly #1; dated

November 6, 2002

NF-AA-310; Move Cover Sheet for Move of Single Rod C-9 From Bundle Q7D210 to the

Temporary Storage Basket; dated June 7, 2002

NF-AA-310; Special Nuclear Material and Core Component Movement; Revision 6

NF-AA-330; Special Nuclear Material Physical Inventory; Revision 1

LIST OF ACRONYMS USED

ALARA

As Low As Is Reasonably Achievable

ASME

American Society of Mechanical Engineers

CFR

Code of Federal Regulations

DRS

Division of Reactor Safety

gpm

Gallons Per Minute

HEPA

High Efficiency Particulate Air

lb

Pound

LERF

Large Early Release Frequency

NRC

Nuclear Regulatory Commission

PI

Performance Indicator

RWP

Radiation Work Permit

SDP

Significance Determination Process