Letter Sequence Other |
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Initiation
- Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request
- Acceptance
- Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement, Supplement
Administration
- Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance, Withholding Request Acceptance
- Meeting, Meeting, Meeting, Meeting, Meeting
Results
Other: CNL-16-008, Update on Progress of Facility Modifications for MSIV Leak Rate, CNL-18-112, Extended Power Uprate - Flow Induced Vibration Summary Report, CNL-18-124, Extended Power Uprate - Replacement Steam Dryer Final Load Definition and Stress Reports, CNL-18-134, Extended Power Uprate - Replacement Steam Dryer Revised Analysis and Limit Curves Report, ML15282A189, ML16085A301, ML16105A297, ML16105A441, ML16168A026, ML16176A316, ML16189A343, ML17062A390, ML17062A403, ML17181A450
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MONTHYEARML15282A1892015-08-31031 August 2015 ANP-3372NP, Revision 1, Browns Ferry Unit 3 Cycle 19 EPU (120% OLTP) LAR Reference Fuel Cycle Design Project stage: Other ML15282A2252015-08-31031 August 2015 ANP-3409NP, Revision 2, Fuel-Related Emergent Regulatory Issues Project stage: Request ML15282A1822015-08-31031 August 2015 ANP-3403NP, Revision 2, Fuel Uprate Safety Analysis Report for Browns Ferry Units 1, 2, and 3, Attachment 9 Project stage: Request ML15282A1932015-08-31031 August 2015 ANP-3385NP, Revision 1, Mechanical Design Report for Browns Ferry Units 1, 2, and 3 Extended Power Uprate (EPU) ATRIUM-10 Fuel Assemblies, Licensing Report Project stage: Request ML15282A2362015-08-31031 August 2015 NEDO-33824, Revision 0, Engineering Report, Browns Ferry Replacement Steam Dryer Stress Analysis Project stage: Request ML15282A1902015-08-31031 August 2015 ANP-3404NP, Revision 2, Browns Ferry Unit 3 Cycle 19 Representative Reload Analysis at Extended Power Uprate Project stage: Request ML15282A2232015-08-31031 August 2015 ANP-2860NP Revision 2, Supplement 2, Browns Ferry Unit 1 - Summary of Responses to Request for Additional Information, Extension for Use of Atrium 10XM Fuel for Extended Power Uprate Project stage: Supplement ML15282A1882015-08-31031 August 2015 ANP-3342NP, Revision 1, Browns Ferry EPU (120% OLTP) Equilibrium Fuel Cycle Design Project stage: Request ML15282A1872015-08-31031 August 2015 ANP-3384NP, Revision 3, Browns Ferry Units 1, 2 and 3, LOCA-ECCS Analysis MAPLHGR Limits for ATRIUM-10 Fuel (Epu) Project stage: Request ML15282A1852015-08-31031 August 2015 ANP-3378NP, Browns Ferry Units 1, 2 and 3, LOCA-ECCS Analysis MAPLHGR Limits for Atrium 10XM Fuel (Epu) Project stage: Request ML15282A1922015-08-31031 August 2015 ANP-3386NP, Revision 1, Mechanical Design Report for Browns Ferry Units 1, 2 and 3 Extended Power Uprate (EPU) Atrium 10XM Fuel Assemblies, Licensing Report Project stage: Request ML15282A1842015-08-31031 August 2015 ANP-3377NP, Browns Ferry Units 1, 2 and 3 LOCA Break Spectrum Analysis Atrium 10XM Fuel (Epu) Project stage: Request ML15282A1522015-09-21021 September 2015 Submits Proposed Technical Specifications Change TS-505 - Request for License Amendments - Extended Power Uprate Project stage: Request ML15282A2402015-09-21021 September 2015 Startup Test Plan Project stage: Request ML15282A2222015-09-21021 September 2015 Cycle 19 MCPR Safety Limit Analysis with SAFLIM3D Methodology Project stage: Request ML15282A2412015-09-21021 September 2015 List and Status of Plant Modifications Project stage: Request ML15282A1812015-09-21021 September 2015 Non-Proprietary - Safety Analysis Report for Browns Ferry, Units 1, 2 and 3, Extended Power Uprate, Attachment 7 Project stage: Request ML15282A2352015-09-21021 September 2015 RHR Heat Exchange K-values Utilities in EPU Containment Analyses Project stage: Request 05000259/LER-2015-002, Regarding High Pressure Coolant Injection System Inoperable Due to Slow Containment Isolation Valve Closing Time2015-09-21021 September 2015 Regarding High Pressure Coolant Injection System Inoperable Due to Slow Containment Isolation Valve Closing Time Project stage: Request CNL-15-249, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 1, Spent Fuel Pool Criticality Safety Analysis Information2015-12-15015 December 2015 Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 1, Spent Fuel Pool Criticality Safety Analysis Information Project stage: Supplement CNL-15-250, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 2, MICROBURN-B2 Information, Including Enclosures 2, 4, 6, and 72015-12-15015 December 2015 Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 2, MICROBURN-B2 Information, Including Enclosures 2, 4, 6, and 7 Project stage: Supplement CNL-15-261, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 3, Interconnection System Impact Study Information2015-12-18018 December 2015 Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 3, Interconnection System Impact Study Information Project stage: Supplement ML16032A0442016-02-0101 February 2016 Fws to NRC, Updated List of Threatened and Endangered Species That May Occur in Your Proposed Project Location for Browns Ferry EPU Project stage: Request ML16041A3072016-02-18018 February 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16040A2322016-02-25025 February 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16041A0222016-02-25025 February 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16049A4632016-02-29029 February 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI CNL-16-045, Proposed Technical Specifications (Ts)Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 6, Response to Request for Additional Information2016-03-0909 March 2016 Proposed Technical Specifications (Ts)Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 6, Response to Request for Additional Information Project stage: Supplement ML16062A0722016-03-15015 March 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI CNL-16-048, Responses to Requests for Additional Information, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU)2016-03-24024 March 2016 Responses to Requests for Additional Information, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) Project stage: Response to RAI ML16084A3202016-03-25025 March 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI CNL-16-055, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 8, Response to Request for Additional Information2016-03-28028 March 2016 Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 8, Response to Request for Additional Information Project stage: Supplement ML16089A1372016-03-29029 March 2016 NRR E-mail Capture - Correction to Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16064A2862016-04-0404 April 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16091A0712016-04-0707 April 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16085A3012016-04-11011 April 2016 Regulatory Audit Plans for April 19 - 21, 2016, Audit at Excel Facility in Rockville, Maryland, in Support of Extended Power Uprate License Amendment Request Project stage: Other CNL-16-069, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 11, Responses to Requests for Additional Information2016-04-14014 April 2016 Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 11, Responses to Requests for Additional Information Project stage: Supplement ML16102A3392016-04-14014 April 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16085A0792016-04-14014 April 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16104A2452016-04-20020 April 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16105A2972016-04-21021 April 2016 Regulatory Audit Plan for May 3-4, 2016, Audit at Excel Facility in Rockville, Maryland, in Support of Extended Power Uprate License Amendment Request Project stage: Other ML16105A4412016-04-27027 April 2016 Regulatory Audit Plan for May 10-11, 2016, Audit at Excel Facility in Rockville, Maryland, in Support of Extended Power Uprate License Amendment Request Project stage: Other CNL-16-077, For Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Update (EPU) - Supplement 14, Response to Request for Additional Information2016-04-27027 April 2016 For Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Update (EPU) - Supplement 14, Response to Request for Additional Information Project stage: Supplement ML16119A4402016-05-0606 May 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate Project stage: RAI ML16119A1332016-05-0606 May 2016 Request for Additional Information Related to License Amendment Request Regarding Extended Power Uprate (SNPB-RAI) Project stage: RAI CNL-16-079, Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 15, Responses to Requests for Additional Information2016-05-11011 May 2016 Proposed Technical Specifications (TS) Change TS-505 - Request for License Amendments - Extended Power Uprate (EPU) - Supplement 15, Responses to Requests for Additional Information Project stage: Supplement ML16120A0722016-05-12012 May 2016 Request for Withholding Information from Public Disclosure Project stage: Withholding Request Acceptance ML16124B1062016-05-12012 May 2016 Request for Withholding Information from Public Disclosure Project stage: Withholding Request Acceptance ML16124A9322016-05-12012 May 2016 Request for Withholding Information from Public Disclosure Project stage: Withholding Request Acceptance ML16123A3352016-05-16016 May 2016 Request for Withholding Information from Public Disclosure Project stage: Withholding Request Acceptance 2016-03-29
[Table View] |
Text
Tennessee Valley Authority, 1101 Market Street, Chattanooga, Tennessee 37402 CNL-16-008 May 26, 2016 10 CFR 50.4 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001 Browns Ferry Nuclear Plant, Units 1, 2, and 3 Renewed Facility Operating License Nos. DPR-33, DPR-52, and DPR-68 NRC Docket Nos. 50-259, 50-260, and 50-296
Subject:
Browns Ferry Nuclear Plant, Units 1, 2, and 3 - Update on Progress of Facility Modifications for MSIV Leak Rate
References:
- 1. TVA letter to NRC, CNL-15-070, Browns Ferry Nuclear Plant, Units 1, 2, and 3 - Withdrawal of Proposed Technical Specification Change to Revise the Leakage Rate Through MSIVs - TS-485, dated May 29, 2015 (ML15159B009)
- 2. TVA letter to NRC, CNL-15-123, Updated Reply to Notice of Violation; EA-11-252; and Follow-up to 10 CFR 50.9, Completeness and accuracy of information, Notification, dated July 15, 2015 (ML15198A353)
In Reference 1, Tennessee Valley Authority (TVA) withdrew a license amendment request (LAR) for the Browns Ferry Nuclear Plant (BFN) Units 1, 2, and 3. The LAR had proposed making the primary alternate leakage (ALT) pathway become the secondary pathway and the secondary pathway would become the credited primary ALT pathway. Additionally, the individual leakage and combined leakage rates through each MSIV would be decreased.
Reference 1 was submitted to the NRC to resolve a non-conforming/degraded condition related to the ALT pathway. In Reference 2, TVA informed the Nuclear Regulatory Commission (NRC) that to resolve the non-conforming/degraded condition, TVA would perform facility and licensing basis modifications such that the current licensing basis dose calculations would remain valid. Additionally, in Reference 1 TVA committed to provide the NRC with an annual status of the progress towards resolving the non-conformance beginning one year from the date of Reference 1 and continuing until the non-conformance has been resolved.
Accordingly, the first annual update of progress of facility modifications is provided below.
U.S. Nuclear Regulatory Commission CNL-16-008 Page 2 May 26, 2016 As described in Enclosure 2 of Reference 2, the proposed facility modifications are as follows.
- 1. "The main steam line (MSL) drain valves FCV-1-168, 169, 170, and 1-171 will either be replaced with fail-open Air Operated Valves (AOVs) with the same valve open control logic for turbine speed < 1700 rpm or the motor operated valve (MOV) breakers will be locked in the open position or these drain valves will be removed. Thus, an open 2" flow path will be assured.
- 2. MOV FCV-1 -58 will be replaced with a fail-open flow control valve. A second valve will be added in a parallel line around FCV-1-58 to avoid single point vulnerability (SPV) in the event that offsite power is not lost during the LOCA.
- 3. TVA will ensure, by design output, that FCV-1-57 is open and that the motive power is removed when the Unit is in Modes 1, 2 or 3."
Engineering analyses and creation of the associated design change packages are in progress.
Date When Full Compliance Will be Achieved The current target schedule for modifying each of the BFN units is during the following outages:
Unit 3: U3R18 Spring 2018 Unit 1: U1R12 Fall 2018 Unit 2: U2R20 Spring 20191 There are no changes to the existing compensatory measures described in Reference 2.
Therefore, if the above target schedule is maintained, full compliance will be achieved following the U2R20 outage scheduled for Spring 2019.
Should you have any questions concerning this submittal, please contact J. L. Paul, Nuclear Site Licensing Manager, at (256) 729-2636.
lly,sl-J.
President, Nuclear Licensing cc: See Page 3 In Enclosure 2 of Reference 2, TVA stated that the modifications for Unit 2 would be completed by March 2017, which was the scheduled date for the U2R19 outage. However, in Enclosure 2 of Reference 2, TVA indicated the possibility that it may be premature to implement the modifications on BFN Unit 2 during the U2R19 outage and that they may be implemented during the next scheduled outage (i.e., U2R20).
U.S. Nuclear Regulatory Commission CNL-16-008 Page 3 May 26, 2016 cc:
NRC Regional Administrator - Region II NRC Senior Resident Inspector - Browns Ferry Nuclear Plant NRR Project Manager - Browns Ferry Nuclear Plant
Tennessee Valley Authority, 1101 Market Street, Chattanooga, Tennessee 37402 CNL-16-008 May 26, 2016 10 CFR 50.4 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001 Browns Ferry Nuclear Plant, Units 1, 2, and 3 Renewed Facility Operating License Nos. DPR-33, DPR-52, and DPR-68 NRC Docket Nos. 50-259, 50-260, and 50-296
Subject:
Browns Ferry Nuclear Plant, Units 1, 2, and 3 - Update on Progress of Facility Modifications for MSIV Leak Rate
References:
- 1. TVA letter to NRC, CNL-15-070, Browns Ferry Nuclear Plant, Units 1, 2, and 3 - Withdrawal of Proposed Technical Specification Change to Revise the Leakage Rate Through MSIVs - TS-485, dated May 29, 2015 (ML15159B009)
- 2. TVA letter to NRC, CNL-15-123, Updated Reply to Notice of Violation; EA-11-252; and Follow-up to 10 CFR 50.9, Completeness and accuracy of information, Notification, dated July 15, 2015 (ML15198A353)
In Reference 1, Tennessee Valley Authority (TVA) withdrew a license amendment request (LAR) for the Browns Ferry Nuclear Plant (BFN) Units 1, 2, and 3. The LAR had proposed making the primary alternate leakage (ALT) pathway become the secondary pathway and the secondary pathway would become the credited primary ALT pathway. Additionally, the individual leakage and combined leakage rates through each MSIV would be decreased.
Reference 1 was submitted to the NRC to resolve a non-conforming/degraded condition related to the ALT pathway. In Reference 2, TVA informed the Nuclear Regulatory Commission (NRC) that to resolve the non-conforming/degraded condition, TVA would perform facility and licensing basis modifications such that the current licensing basis dose calculations would remain valid. Additionally, in Reference 1 TVA committed to provide the NRC with an annual status of the progress towards resolving the non-conformance beginning one year from the date of Reference 1 and continuing until the non-conformance has been resolved.
Accordingly, the first annual update of progress of facility modifications is provided below.
U.S. Nuclear Regulatory Commission CNL-16-008 Page 2 May 26, 2016 As described in Enclosure 2 of Reference 2, the proposed facility modifications are as follows.
- 1. "The main steam line (MSL) drain valves FCV-1-168, 169, 170, and 1-171 will either be replaced with fail-open Air Operated Valves (AOVs) with the same valve open control logic for turbine speed < 1700 rpm or the motor operated valve (MOV) breakers will be locked in the open position or these drain valves will be removed. Thus, an open 2" flow path will be assured.
- 2. MOV FCV-1 -58 will be replaced with a fail-open flow control valve. A second valve will be added in a parallel line around FCV-1-58 to avoid single point vulnerability (SPV) in the event that offsite power is not lost during the LOCA.
- 3. TVA will ensure, by design output, that FCV-1-57 is open and that the motive power is removed when the Unit is in Modes 1, 2 or 3."
Engineering analyses and creation of the associated design change packages are in progress.
Date When Full Compliance Will be Achieved The current target schedule for modifying each of the BFN units is during the following outages:
Unit 3: U3R18 Spring 2018 Unit 1: U1R12 Fall 2018 Unit 2: U2R20 Spring 20191 There are no changes to the existing compensatory measures described in Reference 2.
Therefore, if the above target schedule is maintained, full compliance will be achieved following the U2R20 outage scheduled for Spring 2019.
Should you have any questions concerning this submittal, please contact J. L. Paul, Nuclear Site Licensing Manager, at (256) 729-2636.
lly,sl-J.
President, Nuclear Licensing cc: See Page 3 In Enclosure 2 of Reference 2, TVA stated that the modifications for Unit 2 would be completed by March 2017, which was the scheduled date for the U2R19 outage. However, in Enclosure 2 of Reference 2, TVA indicated the possibility that it may be premature to implement the modifications on BFN Unit 2 during the U2R19 outage and that they may be implemented during the next scheduled outage (i.e., U2R20).
U.S. Nuclear Regulatory Commission CNL-16-008 Page 3 May 26, 2016 cc:
NRC Regional Administrator - Region II NRC Senior Resident Inspector - Browns Ferry Nuclear Plant NRR Project Manager - Browns Ferry Nuclear Plant