05000263/LER-2005-005, Regarding Inadvertent Engineered Safety Function Actuations During Testing

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Regarding Inadvertent Engineered Safety Function Actuations During Testing
ML051520366
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 06/01/2005
From: Thomas J. Palmisano
Nuclear Management Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-MT-05-036 LER 05-005-00
Download: ML051520366 (4)


LER-2005-005, Regarding Inadvertent Engineered Safety Function Actuations During Testing
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iv), System Actuation
2632005005R00 - NRC Website

text

Monticello Nuclear Generating Plant Operated by Nuclear Management Company, LLC June 1, 2005 L-MT-05-036 10 CFR Part 50.73 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555 Monticello Nuclear Generating Plant Docket No. 50-263 License No. DPR-22 LER 2005-005, Inadvertent Engineered Safety Function Actuations during Testing A Licensee Event Report for this occurrence is attached.

This letter makes no new commitments or changes any existing commitments.

Thomas J. Palmisano Site Vice President, Monticello Nuclear Generating Plant Nuclear Management Company, LLC Enclosure cc:

Administrator, Region III, USNRC Project Manager, Monticello, USNRC Resident Inspector, Monticello, USNRC 2807 West County Road 75

  • Monticello, Minnesota 55362-9637 Telephone: 763-295-5151
  • Fax: 763-295-1454

NRC FORM 366 U.S. NUCLEAR REGULATORY (6-2004)

COMMISSION LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB NO. 3150-0104 EXPIRES 6-30-2007

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

FACILITY NAME (1)

DOCKET NUMBER (2)

PAGE (3)

Monticello Nuclear Generating Plant 05000263 1 of 3 TITLE (4) Inadvertent Engineered Safety Function Actuations during Testing EVENT DATE (5)

LER NUMBER (6)

REPORT DATE (7)

OTHER FACILITIES INVOLVED (8)

MO DAY YEAR YEAR SEQUENTIAL NUMBER REV NO MO DAY YEAR FACILITY NAME DOCKET NUMBER 05000 04 02 2005 2005

- 005
- 00 06 01 2005 FACILITY NAME DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) (11)

MODE (9)

N 20.2201(b) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(B) 50.73(a)(2)(ix)(A)

POWER 20.2201(d) 20.2203(a)(4) 50.73(a)(2)(iii) 50.73(a)(2)(x)

LEVEL (10) 0 20.2203(a)(1) 50.36(c)(1)(i)(A)

X 50.73(a)(2)(iv)(A) 73.71(a)(4) 20.2203(a)(2)(i) 50.36(c)(1)(ii)(A) 50.73(a)(2)(v)(A) 73.71(a)(5) 20.2203(a)(2)(ii) 50.36(c)(2) 50.73(a)(2)(v)(B) 20.2203(a)(2)(iii) 50.46(a)(3)(ii) 50.73(a)(2)(v)(C) 20.2203(a)(2)(iv) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(D) 20.2203(a)(2)(v) 50.73(a)(2)(i)(B) 50.73(a)(2)(vii) 20.2203(a)(2)(vi) 50.73(a)(2)(i)(C) 50.73(a)(2)(viii)(A) 20.2203(a)(3)(i) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(B)

LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER (Include Area Code)

Ron Baumer 763-295-1357 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

CAUSE

SYSTEM COMPONENT MANU-FACTURER REPORTABLE TO EPIX

CAUSE

SYSTEM COMPONENT MANU-FACTURER REPORTABLE TO EPIX SUPPLEMENTAL REPORT EXPECTED (14)

MONTH DAY YEAR YES (If yes, complete EXPECTED SUBMISSION DATE).

X NO EXPECTED SUBMISSION DATE (15)

ABSTRACT On April 2, 2005 at 1648, Operations was performing a Post Maintenance Test (PMT) in accordance with a procedure, following replacement of a relay. During the performance of the procedure, the #16 4KV Safety Related Bus was de-energized. Operations entered the appropriate procedures for the loss of Bus 16, and power was restored at 2140. A review of the event determined that the PMT procedure did not contain the correct steps to permit the test to be successfully completed. This resulted in a knife switch being left in the open position that caused a relay to sense a loss of bus voltage, even though the voltage was actually available. This caused the bus transfer logic to seek a new source of power that resulted in Bus 16 de-energizing.

The Root Cause Evaluation determined that the procedures for preparation, review and approval of complex PMTs lack sufficient detail with respect to responsibilities and actions required. Corrective actions planned or completed include: restoration of the bus, and planned revision of station procedures regarding the development and review process for PMTs.

OTHER Specify in Abstract below or in NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION (1-2001)

LICENSEE EVENT REPORT (LER)

FACILITY NAME (1)

DOCKET (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL NUMBER REVISION NUMBER Monticello Nuclear Generating Plant 05000263 2005 005 00 2 of 3 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) Description On April 2, 2005, with the reactor shutdown during a refueling outage and Residual Heat Removal (RHR) [BO] providing shutdown cooling, Operations personnel were performing a Post Maintenance Test (PMT) in accordance with a procedure, following replacement of a relay [RLY]. At 1648, during the performance of the procedure, the number 16 4KV [EA] Safety Related Bus [BU] was unexpectedly de-energized. The de-energizing of Bus 16 resulted in a loss of the loads off the bus including Load Center [SSBU] 104, Motor Control Center [SSBU] 141, and Reactor Protection System (RPS) [JD] bus B (and associated loads). Due to the event the following safety systems were actuated: the reactor building ventilation [VA] isolated, A Standby Gas Treatment System (SBGTS) [JE] initiated, the A Control Room Emergency Filtration Train (EFT) [VI] initiated, and the Reactor Water Cleanup System (RWCU) [CE] tripped. In addition the B RPS logic initiated a half scram.

Operations entered the appropriate procedures for the loss of Bus 16, and power was restored at 2140.

A review of the event determined that the PMT procedure did not contain the correct steps to permit the test to be successfully completed. This resulted in a knife switch being left in the open position that caused a relay to sense a loss of bus voltage, even though the voltage was actually available. This caused the bus transfer logic to seek a new source of power that resulted in bus 16 de-energizing. The procedure was revised and the PMT was re-performed; subsequent testing proved successful.

Event Analysis

The knife switch being left in the open position caused the relay to sense a loss of bus voltage, even though the voltage was actually available. Therefore, the ESF actuations were the result of an invalid actuation signal and in accordance with NUREG-1022, no notification under 10 CFR 50.72 was required. Per 10 CFR 50.73 (a)(2)(iv), a Licensee Event report is required for this event since the system was not properly removed from service.

The event is not classified as a safety system functional failure.

Safety Significance

The de-energizing of bus 16 resulted in a loss of the loads off the bus and loss of Load Center 104, Motor Control Center 141, and RPS bus B (and associated loads). The impact on the plant was minor since shutdown cooling (SDC) was not lost and reactor temperature did not increase.

Operators were notified of the loss by annunciator 8-C-19, No. 14 4160V Bus to No. 16 Bus Breaker Trip. The Annunciator Response Procedure for this alarm directs the Operators to perform the procedure for Loss of Bus 15 or Bus 16. Bus 16 was restored following completion of the procedure, and the cause understood and corrected. All safety related equipment performed as expected.

The Probabilistic Risk Assessment (PRA) group performed an evaluation for significance. The change in Core Damage Frequency (CDF) after crediting the available recovery methods was 6.56 x 10-9. In addition, SDC was not lost so decay heat removal was not affected. This event had low significance. U.S. NUCLEAR REGULATORY COMMISSION (1-2001)

LICENSEE EVENT REPORT (LER)

FACILITY NAME (1)

DOCKET (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL NUMBER REVISION NUMBER Monticello Nuclear Generating Plant 05000263 2005 005 00 3 of 3 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

Cause

The Root Cause Evaluation determined that the procedures for preparation, review and approval of complex PMTs lack sufficient detail with respect to responsibilities and actions required.

Corrective Action

Operations restored Bus 16 using the appropriate operating procedures.

As an interim action, the site increased the review expectations for PMTs. All PMTs that used portions of approved surveillance procedures were required to have a technical review and Senior Reactor Operator review prior to implementation.

Site procedures will be revised to provide more formal control of the PMT development process. The revised process will incorporate a graded approach for development of PMTs and apply the necessary level of reviews in an effort to prevent further events.

Failed Component Identification N/A

Previous Similar Events

No station Licensee Event Reports were found that were similar to the events in this LER. However, one station corrective action report (CAP), CAP035444, identified that inadequate reviews were performed for a specific PMT. This was attributed to inattention to detail by reviewers and was closed by correcting the PMT.