ML093230675
| ML093230675 | |
| Person / Time | |
|---|---|
| Site: | Waterford |
| Issue date: | 11/18/2009 |
| From: | Clark J NRC/RGN-IV/DRP/RPB-E |
| To: | Kowalewski J Entergy Operations |
| References | |
| IR-09-004 | |
| Download: ML093230675 (35) | |
See also: IR 05000382/2009004
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
R E GI ON I V
612 EAST LAMAR BLVD, SUITE 400
ARLINGTON, TEXAS 76011-4125
November 18, 2009
Joseph Kowalewski, Vice President, Operations
Entergy Operations, Inc.
Waterford Steam Electric Station, Unit 3
17265 River Road
Killona, LA 70057-3093
Subject:
WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC INTEGRATED
INSPECTION REPORT 05000382/2009-004
Dear Mr. Kowalewski:
On October 7, 2009, the U.S. Nuclear Regulatory Commission completed an inspection at your
Waterford Steam Electric Station, Unit 3. The enclosed integrated inspection report documents
the inspection findings, which were discussed on October 1, 2009, with you and other members
of your staff.
The inspections examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents one NRC identified finding of very low safety significance (Green). This
finding was determined to involve a violation of NRC requirements. However, because of the
very low safety significance and because it was entered into your corrective action program, the
NRC is treating this finding as a noncited violation, consistent with Section VI.A.1 of the NRC
Enforcement Policy. If you contest the violation or the significance of the noncited violation, you
should provide a response within 30 days of the date of this inspection report, with the basis for
your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear
Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas,
76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,
Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Waterford Steam Electric
Station, Unit 3 facility. In addition, if you disagree with the characterization of any finding in this
report, you should provide a response within 30 days of the date of this inspection report, with
the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC
Resident Inspector at Waterford Steam Electric Station, Unit 3. The information you provide will
be considered in accordance with Inspection Manual chapter 0305.
Entergy Operations, Inc.
- 2 -
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its
enclosure, will be available electronically for public inspection in the NRC Public Document
Room or from the Publicly Available Records component of NRCs document system (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the
Public Electronic Reading Room).
Sincerely,
/RA/
Jeffrey A. Clark, P.E.
Chief, Project Branch E
Division of Reactor Projects
Docket: 50-382
License: NPF-38
Enclosure:
NRC Inspection Report 05000382/2009004
w/Attachment: Supplemental Information
cc w/Enclosure:
Senior Vice President
Entergy Nuclear Operations
P.O. Box 31995
Jackson, MS 39286-1995
Senior Vice President and
Chief Operating Officer
Entergy Operations, Inc.
P.O. Box 31995
Jackson, MS 39286-1995
Vice President, Operations Support
Entergy Services, Inc.
P.O. Box 31995
Jackson, MS 39286-1995
Senior Manager, Nuclear Safety
and Licensing
Entergy Services, Inc.
P.O. Box 31995
Jackson, MS 39286-1995
Site Vice President
Waterford Steam Electric Station, Unit 3
Entergy Operations, Inc.
17265 River Road
Killona, LA 70057-0751
Entergy Operations, Inc.
- 3 -
Director
Nuclear Safety Assurance
Entergy Operations, Inc.
17265 River Road
Killona, LA 70057-0751
General Manager, Plant Operations
Waterford 3 SES
Entergy Operations, Inc.
17265 River Road
Killona, LA 70057-0751
Manager, Licensing
Entergy Operations, Inc.
17265 River Road
Killona, LA 70057-3093
Chairman
Louisiana Public Service Commission
P.O. Box 91154
Baton Rouge, LA 70821-9154
Parish President Council
St. Charles Parish
P.O. Box 302
Hahnville, LA 70057
Director, Nuclear Safety & Licensing
Entergy, Operations, Inc.
440 Hamilton Avenue
White Plains, NY 10601
Louisiana Department of Environmental
Quality, Radiological Emergency Planning
and Response Division
P.O. Box 4312
Baton Rouge, LA 70821-4312
Chief, Technological Hazards Branch
FEMA Region VI
800 North Loop 288
Federal Regional Center
Denton, TX 76209
Entergy Operations, Inc.
- 4 -
Electronic distribution by RIV:
Regional Administrator (Elmo.Collins@nrc.gov)
Deputy Regional Administrator (Chuck.Casto@nrc.gov)
DRP Director (Dwight.Chamberlain@nrc.gov)
DRP Deputy Director (Anton.Vegel@nrc.gov)
DRS Director (Roy.Caniano@nrc.gov)
DRS Deputy Director (Troy.Pruett@nrc.gov)
Senior Resident Inspector (Mark.Haire@nrc.gov)
Resident Inspector (Dean.Overland@nrc.gov)
Branch Chief, DRP/E (Jeff.Clark@nrc.gov)
Senior Project Engineer, DRP/E (Ray.Azua@nrc.gov)
WAT Site Secretary (Linda.Dufrene@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)
Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
OEMail Resource
Regional State Liaison Officer (Bill.Maier@nrc.gov)
NSIR/DPR/EP (Steve.LaVie@nrc.gov)
OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)
ROPreports
File located: R:\\_REACTORS\\_WAT\\2009\\WAT 2009004 RP-DHO.doc
SUNSI Rev Compl.
- Yes No
- Yes No
Reviewer Initials
Publicly Avail
- Yes No
Sensitive
Yes : No
Sens. Type Initials
RIV:SRI:DRP/E
SPE/DRP/E
C:DRS/EB1
C:DRS/EB2
DHOverland
RAzua
TRFarnholtz
NFOKeefe
/RA/RAzua for
/RA/
/RA/
/RA/
11/17/09
11/17/09
11/12/09
11/12/09
C:DRS/OB
C:DRS/PSB1
C:DRS/PSB2
C:DRP/E
SGarchow
MPShannon
GEWerner
JAClark
/RA/
/RA/
/RA/
/RA/RAzua for
11/17/2009
11/13/09
E11/11/09
11/17/09
OFFICIAL RECORD COPY
T=Telephone E=E-mail
F=Fax
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket:
05000382
License:
NFP-38
Report:
Licensee:
Entergy Operations, Inc.
Facility:
Waterford Steam Electric Station, Unit 3
Location:
Hwy. 18
Killona, LA
Dates:
July 8, 2009 through October 7, 2009
Inspectors:
D. Overland, Senior Resident Inspector
R. Egli, Branch Chief, TTC
R. Hickok, Senior Reactor Technology Instructor, TTC
G. Replogle, Senior Project Engineer, RIV
M. Chambers, Resident Inspector, Cooper Nuclear Station
P. Jayroe, Project Engineer, RIV
T. Buchanan, Project Engineer, RIV
S. Anderson, General Engineer, HQ
L. Carson II, Senior Health Physicist
Approved By:
Jeff Clark, Chief, Project Branch E
Division of Reactor Projects
- 1 -
Enclosure
SUMMARY OF FINDINGS
IR 05000382/2009004; July 8, 2009 through October 7, 2009; Waterford Steam Electric Station,
Unit 3; Operability Evaluations.
The report covered a 3-month period of inspection by resident inspectors and announced
baseline inspections by regional based inspectors. One Green noncited violation of significance
was identified. The significance of most findings is indicated by their color (Green, White,
Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process.
Findings for which the significance determination process does not apply may be Green or be
assigned a severity level after NRC management review. The NRC's program for overseeing
the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
Oversight Process, Revision 4, dated December 2006.
A.
NRC-Identified Findings and Self-Revealing Findings
Cornerstone: Mitigating Systems
Green. The inspectors identified a Green non-cited violation of technical specification 3.3.1, Reactor Protective Instrumentation. The technical specifications require all four
channels (A, B, C, and D) of local power density, departure from nucleate boiling ratio,
and reactor coolant flow instruments to be operable when in Mode 1. These Channel B
instruments require an input from the Channel B log power instrument, which was
previously declared inoperable. With the Channel B log power instrument inoperable,
the Channel B local power density, departure from nucleate boiling ratio, and reactor
coolant flow instruments should also have been declared inoperable. The licensee
entered this finding in their corrective action program as condition reports CR-WF3-
2009-4401 and CR-WF3-2009-4407.
The failure to either trip or bypass the inoperable channels within one hour was more
than minor because it affected the configuration control attribute of the mitigating
systems cornerstone. Specifically, deliberate operator action was required to ensure that
proper reactor protection system coincidence and reliability were maintained. Also, if left
uncorrected, the potential existed for Channel B reactor protective trips to be
inadvertently removed while at power. The failure to meet the technical specifications
was considered to be of very low safety significance (Green), since there was no actual
loss of safety function. This finding has a cross-cutting aspect in the decision-making
component of the human performance area because the licensee failed to verify the
validity of underlying assumptions and identify unintended consequences of failing to
comply with technical specification 3.3.1 by declaring the log power Channel B
inoperable and not placing local power density, departure from nucleate boiling ratio,
and reactor coolant flow instrument channels in either bypass or trip condition (H.1.b).
(Section 1R15)
B.
Licensee-Identified Violations
None
- 2 -
Enclosure
REPORT DETAILS
Summary of Plant Status
The plant began the inspection period on July 8, 2009, at 100 percent power and remained at
approximately 100 percent power for the rest of the inspection period.
1.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and
1R01 Adverse Weather Protection (71111.01)
.1
Readiness for Impending Adverse Weather Conditions
a.
Inspection Scope
Since thunderstorms with potential tornados and high winds were forecast in the vicinity
of the facility for October 4, 2009, the inspectors reviewed the licensees overall
preparations/protection for the expected weather conditions. The inspectors evaluated
the licensee staffs documented preparations against the sites procedures and
determined that the staffs actions were adequate. During the inspection, the inspectors
focused on plant-specific design features and the licensees procedures used to respond
to specified adverse weather conditions. The inspector's evaluated operator staffing and
accessibility of controls and indications for those systems required to control the plant.
Additionally, the inspectors reviewed the Updated Final Safety Analysis Report and
verified that operator actions were appropriate as specified by plant-specific procedures.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one readiness for impending adverse weather
condition sample as defined in Inspection Procedure 71111.01-05.
b.
Findings
No findings of significance were identified.
1R04 Equipment Alignments (71111.04)
.1
Partial Walkdown
a.
Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant
systems:
July 22, 2009: Chemical volume control Train A
August 12, 2009: Emergency feedwater Train A
August 13, 2009: Low pressure safety injection Train B
August 18, 2009: Emergency feedwater Train AB
September 15, 2009: High pressure safety injection system Train A
- 3 -
Enclosure
The inspectors selected these systems based on their risk significance relative to the
reactor safety cornerstones at the time they were inspected. The inspectors attempted
to identify any discrepancies that could affect the function of the system, and, therefore,
potentially increase risk. The inspectors reviewed applicable operating procedures,
system diagrams, Updated Final Safety Analysis Report, technical specification
requirements, administrative technical specifications, outstanding work orders, condition
reports, and the impact of ongoing work activities on redundant trains of equipment in
order to identify conditions that could have rendered the systems incapable of
performing their intended functions. The inspectors also walked down accessible
portions of the systems to verify system components and support equipment were
aligned correctly and operable. The inspectors examined the material condition of the
components and observed operating parameters of equipment to verify that there were
no obvious deficiencies. The inspectors also verified that the licensee had properly
identified and resolved equipment alignment problems that could cause initiating events
or impact the capability of mitigating systems or barriers and entered them into the
corrective action program with the appropriate significance characterization. Specific
documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of five partial system walkdown samples as
defined in Inspection Procedure 71111.04-05.
b.
Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05)
.1
Quarterly Fire Inspection Tours
a.
Inspection Scope
The inspectors conducted fire protection walkdowns that were focused on availability,
accessibility, and the condition of firefighting equipment in the following risk-significant
plant areas:
July 21, 2009: Reactor auxiliary building fire Zones 8B, 8C, 11, and 12
July 22, 2009: Reactor auxiliary building fire Zones 33, 35, 38, and 39
July 30, 2009: Reactor auxiliary building fire Zones 3, 5, and 6
August 3, 2009: Fire Zones Roof E and Roof W
August 11, 2009: Reactor auxiliary building fire Zone 16
August 18, 2009: Reactor auxiliary building fire Zones 33, 35, 36, 37, 38, and 39
August 19, 2009: Reactor auxiliary building fire Zone 32
August 20, 2009: Reactor auxiliary building fire Zones 2, Roof E, and Roof W
August 23, 2009: Reactor auxiliary building fire Zones 11, 12,13, 8B, and 8C
August 24, 2009: Reactor auxiliary building fire Zones 15, 16, 17, 18, 19, 20,
and 21
The inspectors reviewed areas to assess if licensee personnel had implemented a fire
protection program that adequately controlled combustibles and ignition sources within
- 4 -
Enclosure
the plant; effectively maintained fire detection and suppression capability; maintained
passive fire protection features in good material condition; and had implemented
adequate compensatory measures for out of service, degraded or inoperable fire
protection equipment, systems, or features, in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk
as documented in the plants Individual Plant Examination of External Events with later
additional insights, their potential to affect equipment that could initiate or mitigate a plant
transient, or their impact on the plants ability to respond to a security event. Using the
documents listed in the attachment, the inspectors verified that fire hoses and
extinguishers were in their designated locations and available for immediate use; that
fire detectors and sprinklers were unobstructed, that transient material loading was
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
be in satisfactory condition. The inspectors also verified that minor issues identified
during the inspection were entered into the licensees corrective action program.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of ten quarterly fire-protection inspection samples
as defined in Inspection Procedure 71111.05-05.
b.
Findings
No findings of significance were identified.
.2
Annual Fire Protection Drill Observation (71111.05A)
a.
Inspection Scope
On September 23, 2009, the inspectors observed a fire brigade activation as the result
of a simulated fire at feed heater drain Pump C. The observation evaluated the
readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee
staff identified deficiencies, openly discussed them in a self-critical manner at the drill
debrief, and took appropriate corrective actions. Specific attributes evaluated were:
(1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper
use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;
(4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade
leader communications, command, and control; (6) search for victims and propagation of
the fire into other plant areas; (7) smoke removal operations; (8) utilization of pre
planned strategies; (9) adherence to the preplanned drill scenario; and (10) drill
objectives.
These activities constitute completion of one annual fire-protection inspection sample as
defined in Inspection Procedure 71111.05-05.
b.
Findings
No findings of significance were identified.
- 5 -
Enclosure
1R11 Licensed Operator Requalification Program (71111.11)
a.
Inspection Scope
On August 4, 2009, the inspectors observed a crew of licensed operators in the plants
simulator to verify that operator performance was adequate, evaluators were identifying
and documenting crew performance problems, and training was being conducted in
accordance with licensee procedures. The inspectors evaluated the following areas:
Licensed operator performance
Crews clarity and formality of communications
Crews ability to take timely actions in the conservative direction
Crews prioritization, interpretation, and verification of annunciator alarms
Crews correct use and implementation of abnormal and emergency procedures
Control board manipulations
Oversight and direction from supervisors
Crews ability to identify and implement appropriate technical specification actions
and emergency plan actions and notifications
The inspectors compared the crews performance in these areas to pre-established
operator action expectations and successful critical task completion requirements.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one quarterly licensed-operator requalification
program sample as defined in Inspection Procedure 71111.11.
b.
Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12Q)
a.
Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk
significant systems:
August 11, 2009: Seal leakage on chemical volume control charging pumps
September 3, 2009: Review of operating experience smart sample FY 2009-01,
Inspection of electrical connections for motor control center, circuit breakers and
interfaces
- 6 -
Enclosure
The inspectors reviewed events such as where ineffective equipment maintenance has
resulted in valid or invalid automatic actuations of engineered safeguards systems and
independently verified the licensee's actions to address system performance or condition
problems in terms of the following:
Implementing appropriate work practices
Identifying and addressing common cause failures
Scoping of systems in accordance with 10 CFR 50.65(b)
Characterizing system reliability issues for performance
Charging unavailability for performance
Trending key parameters for condition monitoring
Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)
Verifying appropriate performance criteria for structures, systems, and
components classified as having an adequate demonstration of performance
through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as
requiring the establishment of appropriate and adequate goals and corrective
actions for systems classified as not having adequate performance, as described
The inspectors assessed performance issues with respect to the reliability, availability,
and condition monitoring of the system. In addition, the inspectors verified maintenance
effectiveness issues were entered into the corrective action program with the appropriate
significance characterization. Specific documents reviewed during this inspection are
listed in the attachment.
These activities constitute completion of two quarterly maintenance effectiveness
samples as defined in Inspection Procedure 71111.12-05.
b.
Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
a.
Inspection Scope
The inspectors reviewed licensee personnel's evaluation and management of plant risk
for the maintenance and emergent work activities affecting risk-significant and safety-
related equipment listed below to verify that the appropriate risk assessments were
performed prior to removing equipment for work:
July 29, 2009: Scheduled elective maintenance outage for containment fan
coolers Train B to calibrate containment fan cooler Header B CCW return
temperature control valve solenoid Valve CC-835B
- 7 -
Enclosure
August 3, 2009: Scheduled surveillance of reactor protection system Channel A
September 9, 2009: Scheduled activity to remove high pressure safety injection
Pump AB from high pressure safety injection Train A alignment and align high
pressure safety injection Pump A to Train A
September 11, 2009: Emergent maintenance to replace station Battery AB,
Cell 31 with a spare cell due to degraded cell voltage
The inspectors selected these activities based on potential risk significance relative to
the reactor safety cornerstones. As applicable for each activity, the inspectors verified
that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)
and that the assessments were accurate and complete. When licensee personnel
performed emergent work, the inspectors verified that the licensee personnel promptly
assessed and managed plant risk. The inspectors reviewed the scope of maintenance
work, discussed the results of the assessment with the licensee's probabilistic risk
analyst or shift technical advisor, and verified plant conditions were consistent with the
risk assessment. The inspectors also reviewed the technical specification requirements
and inspected portions of redundant safety systems, when applicable, to verify risk
analysis assumptions were valid and applicable requirements were met. Specific
documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of four maintenance risk assessments and
emergent work control inspection samples as defined in Inspection
Procedure 71111.13-05.
b.
Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a.
Inspection Scope
The inspectors reviewed the following issues:
July 14, 2009: Low individual cell voltage on vital 125 vdc station Battery AB
Cell 39
August 11, 2009: Unplanned load variations during emergency diesel generator
Train A surveillance
August 12, 2009: Emergency diesel generator Train A Relay EG EREL 2342(J)
found out of calibration during surveillance
August 20, 2009: Channel B local power density, departure from nucleate boiling
ratio, and reactor coolant flow instruments, when Channel B log power
instrument was inoperable
- 8 -
Enclosure
The inspectors selected these potential operability issues based on the risk-significance
of the associated components and systems. The inspectors evaluated the technical
adequacy of the evaluations to ensure that technical specification operability was
properly justified and the subject component or system remained available such that no
unrecognized increase in risk occurred. The inspectors compared the operability and
design criteria in the appropriate sections of the technical specifications and Updated
Safety Analysis Report to the licensees evaluations, to determine whether the
components or systems were operable. Where compensatory measures were required
to maintain operability, the inspectors determined whether the measures in place would
function as intended and were properly controlled. The inspectors determined, where
appropriate, compliance with bounding limitations associated with the evaluations.
Additionally, the inspectors also reviewed a sampling of corrective action documents to
verify that the licensee was identifying and correcting any deficiencies associated with
operability evaluations. Specific documents reviewed during this inspection are listed in
the attachment.
These activities constitute completion of four operability evaluations inspection samples
as defined in Inspection Procedure 71111.15-05
b.
Findings
Introduction: The inspectors identified a Green non-cited violation of technical
specification 3.3.1, Reactor Protective Instrumentation. The technical specifications
require all four channels (A, B, C, and D) of local power density, departure from nucleate
boiling ratio, and reactor coolant flow instruments to be operable when in Mode 1.
These Channel B instruments require an input from the Channel B log power instrument,
which was previously declared inoperable. With the Channel B log power instrument
inoperable, the Channel B local power density, departure from nucleate boiling ratio, and
reactor coolant flow instruments should also have been declared inoperable.
Description: On Aug 20, 2009, the inspector observed the performance of procedure
MI-003-126, Revision 14, Core Protection Calculator Functional. During the
performance of the test procedure, the inspector noted that CPC Channel B high log
power trip was bypassed. The inspector asked why technical specification 3.3.1 had not
been entered due to the inoperable log power Channel B instrument. Technical
specification 3.3.1, Reactor Protective Instrumentation, requires that the reactor
protective instrumentation channels and bypasses contained in Table 3.3-1 be operable
in accordance with the requirements of the table. Table 3.3-1 requires all four channels
of local power density (LPD), departure from nucleate boiling ratio (DNBR), and reactor
coolant flow instruments to be operable in Mode 1.
Log power Channel B provides a high log power automatic bypass removal signal for
LPD, DNBR, and reactor coolant flow instrumentation channels. Technical specification 3.3.1, Table 3.3-1 requires the high log power bypass shall be automatically removed
when reactor power is greater than or equal to 10-4% of rated thermal power. When in
Mode 1, reactor power is greater than 10-4% of rated thermal power. The inspectors
determined that when a log power instrument is out of service, the automatic removal of
the high log power bypass function is inoperable and thus the associated protective
channels of LPD, DNBR, and reactor coolant flow are also inoperable.
- 9 -
Enclosure
The log power Channel B instrument was originally declared inoperable on Sept 1, 2008.
The operability determination concluded that since the plant was in Mode 4, only two log
power channels were required, therefore entry into technical specification 3.3.1 was not
required. On Sept 9, 2008, the plant entered Mode 2 with log power Channel B still
inoperable. The operability was not revised to reflect the change in plant conditions. In
accordance with technical specification 3.3.1, operators should have taken action to
place the associated LPD, DNBR, and reactor coolant flow protective channels to either
bypass or trip within one hour.
On Aug 22, 2009, after considering the inspectors question, the licensee declared LPD
Channel B and DNBR Channel B inoperable, and placed both instruments in bypass.
During a subsequent control room tour, the inspector verified that LPD and DNBR were
bypassed, however noticed that reactor coolant flow Channel B had not been bypassed.
The inspector asked the shift manager if technical specification 3.3.1, Table 3.3-1
notation (C) affected any other trips. Upon further assessment, operations personnel
determined that reactor coolant low flow was also affected and declared steam
generator flow Channel B to be inoperable, as well.
Analysis: The failure to either trip or bypass the inoperable channels within one hour
was more than minor because it affected the configuration control attribute of the
mitigating systems cornerstone. Specifically, deliberate operator action was required to
ensure that proper reactor protection system coincidence and reliability were maintained.
Also, if left uncorrected, the potential existed for Channel B reactor protective trips to be
inadvertently removed while at power. The failure to meet the technical specifications
was considered to be of very low safety significance (Green), since there was no actual
loss of safety function. This finding has a cross-cutting aspect in the decision-making
component of the human performance area because the licensee failed to verify the
validity of underlying assumptions and identify unintended consequences of failing to
comply with technical specification 3.3.1 by declaring the log power Channel B
inoperable and not placing DNBR, LPD, and reactor coolant flow channels in either
bypass or trip condition (H.1.b).
Enforcement: Technical specification 3.3.1, Reactor Protective Instrumentation,
requires all four channels of LPD, DNBR, and reactor coolant flow to be operable and
able to have the high log power bypass automatically removed when reactor power is
greater than or equal to 10-4% percent of rated thermal power. Contrary to this, on
September 9, 2008, the licensee did not comply with the limiting condition for operation
action statement for technical specification 3.3.1 which states, the inoperable channel is
placed in either the bypassed or tripped condition within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. The plant remained in
this condition until August 22, 2009. This violation has been determined to be of very
low safety significance and was entered into their corrective action program in condition
reports CR-WF3-2009-4401 and CR-WF3-2009-4407. Therefore, this violation is being
treated as a non-cited violation (NCV), consistent with Section VI.A.1 of the NRC
- 10 -
Enclosure
1R18 Plant Modifications (71111.18)
a.
Inspection Scope
The inspectors reviewed the following temporary/permanent modifications to verify that
the safety functions of important safety systems were not degraded:
August 26, 2009: Permanent modification of containment vacuum relief valves
such that once the valves are automatically opened, they remain open until
manually closed.
August 7, 2009: Temporary modification to revise the setpoint for the reactor
coolant Pump 2A upper thrust bearing high temperature alarm to reduce
nuisance alarms in the control room.
September 14, 2009: Temporary modification to replace station Battery AB, Cell
31 with a new cell. The old Cell 31 was left in place and jumpered around, while
the new Cell 31 was installed at the end of the battery rack.
The inspectors reviewed the temporary modification and the associated safety
evaluation screening against the system design bases documentation, including the
Updated Final Safety Analysis Report and the technical specifications, and verified that
the modification did not adversely affect the system operability/availability. The
inspectors also verified that the installation and restoration were consistent with the
modification documents and that configuration control was adequate. Additionally, the
inspectors verified that the temporary modification was identified on control room
drawings, appropriate tags were placed on the affected equipment, and licensee
personnel evaluated the combined effects on mitigating systems and the integrity of
radiological barriers.
The inspectors reviewed key affected parameters associated with energy needs,
materials/replacement components, timing, heat removal, control signals, equipment
protection from hazards, operations, flow paths, pressure boundary, ventilation
boundary, structural, process medium properties, licensing basis, and failure modes for
the modification listed below. The inspectors verified that modification preparation,
staging, and implementation did not impair emergency/abnormal operating procedure
actions, key safety functions, or operator response to loss of key safety functions;
postmodification testing will maintain the plant in a safe configuration during testing by
verifying that unintended system interactions will not occur, systems, structures and
components performance characteristics still meet the design basis, the
appropriateness of modification design assumptions, and the modification test
acceptance criteria will be met; and licensee personnel identified and implemented
appropriate corrective actions associated with permanent plant modifications. Specific
documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of three samples for temporary and permanent
plant modifications as defined in Inspection Procedure 71111.18-05
- 11 -
Enclosure
b.
Findings
No findings of significance were identified.
1R19 Postmaintenance Testing (71111.19)
a.
Inspection Scope
The inspectors reviewed the following postmaintenance activities to verify that
procedures and test activities were adequate to ensure system operability and functional
capability:
June 23, 2009: Replacement of high pressure safety injection Pump B Tyco time
delay relay following the failure of the relay to start the pump during a routine
surveillance test
July 23, 2009: Replacement of seal package on chemical volume control
charging Pump B to reduce reactor coolant system unidentified leakage
July 29, 2009: Scheduled elective maintenance calibration of containment fan
cooler Header B CCW return temperature control valve solenoid Valve CC-835B
August 4, 2009: Corrective maintenance to repair the actuator for steam
generator SG1 main steam atmospheric dump Valve MS-116A
August 11, 2009: Scheduled preventative maintenance to clean, inspect, and
test emergency diesel generator Train A Relay EG EREL 2342(J)
September 9, 2009: Scheduled preventative maintenance to replace the
pulsation dampener and perform motor maintenance on chemical volume control
charging Pump AB
September 14, 2009: Emergent maintenance to replace station Battery AB,
Cell 31 with a spare cell, due to degraded voltage on the cell
September 29, 2009: Scheduled preventative maintenance to check the
overcurrent trip on the breaker for non-nuclear safety return header isolation
Valve CC-562.
The inspectors selected these activities based upon the structure, system, or
component's ability to affect risk. The inspectors evaluated these activities for the
following (as applicable):
The effect of testing on the plant had been adequately addressed; testing was
adequate for the maintenance performed
Acceptance criteria were clear and demonstrated operational readiness; test
instrumentation was appropriate
- 12 -
Enclosure
The inspectors evaluated the activities against the technical specifications, the Updated
Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and
various NRC generic communications to ensure that the test results adequately ensured
that the equipment met the licensing basis and design requirements. In addition, the
inspectors reviewed corrective action documents associated with postmaintenance tests
to determine whether the licensee was identifying problems and entering them in the
corrective action program and that the problems were being corrected commensurate
with their importance to safety. Specific documents reviewed during this inspection are
listed in the attachment.
These activities constitute completion of eight postmaintenance testing inspection
sample(s) as defined in Inspection Procedure 71111.19-05.
b.
Findings
No findings of significance were identified.
1R22 Surveillance Testing (71111.22)
a.
Inspection Scope
The inspectors reviewed the Updated Final Safety Analysis Report, procedure
requirements, and technical specifications to ensure that the six surveillance activities
listed below demonstrated that the systems, structures, and/or components tested were
capable of performing their intended safety functions. The inspectors either witnessed or
reviewed test data to verify that the significant surveillance test attributes were adequate
to address the following:
Preconditioning
Evaluation of testing impact on the plant
Acceptance criteria
Test equipment
Procedures
Jumper/lifted lead controls
Test data
Testing frequency and method demonstrated technical specification operability
Test equipment removal
Restoration of plant systems
Fulfillment of ASME Code requirements
- 13 -
Enclosure
Updating of performance indicator data
Engineering evaluations, root causes, and bases for returning tested systems,
structures, and components not meeting the test acceptance criteria were correct
Reference setting data
Annunciators and alarms setpoints
The inspectors also verified that licensee personnel identified and implemented any
needed corrective actions associated with the surveillance testing.
August 6, 2009: Safety related electrical Bus 3A undervoltage relay calibration
August 10, 2009: Emergency diesel generator Train A surveillance
August 20, 2009: Core protection calculator Train B surveillance
August 22, 2009: Plant protection system Channel B surveillance
August 24, 2009: Emergency diesel generator and subgroup relays Train B
September 14, 2009: High pressure safety injection Train AB
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of six surveillance testing inspection samples as
defined in Inspection Procedure 71111.22-05.
b.
Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation (71114.06)
.1
Training Observations
a.
Inspection Scope
The inspectors observed a training evolution for licensed operators on September 17,
2009, which required emergency plan implementation by a licensee operations crew.
This evolution was planned to be evaluated and included in performance indicator data
regarding drill and exercise performance. The inspectors observed event classification
and notification activities performed by the crew. The inspectors also attended the
postevolution critique for the scenario. The focus of the inspectors activities was to note
any weaknesses and deficiencies in the crews performance and ensure that the
licensee evaluators noted the same issues and entered them into the corrective action
program. As part of the inspection, the inspectors reviewed the scenario package and
other documents listed in the attachment.
These activities constitute completion of one sample as defined in Inspection
Procedure 71114.06-05.
- 14 -
Enclosure
b.
Findings
No findings of significance were identified.
2.
RADIATION SAFETY
Cornerstone: Occupational and Public Radiation Safety
2OS2 ALARA Planning and Controls (71121.02)
a.
Inspection Scope
The inspector assessed licensee performance with respect to maintaining individual and
collective radiation exposures ALARA. The inspector used the requirements in 10 CFR
Part 20 and the licensees procedures required by technical specifications as criteria for
determining compliance. The inspector interviewed licensee personnel and reviewed:
Current 3-year rolling average collective exposure
Five outage work activities scheduled during the inspection period and
associated work activity exposure estimates which were likely to result in the
highest personnel collective exposures
Site-specific trends in collective exposures, plant historical data, and source-term
measurements
Five work activities of highest exposure significance completed during the last
outage
ALARA work activity evaluations, exposure estimates, and exposure mitigation
requirements
Intended versus actual work activity doses and the reasons for any
inconsistencies
Person-hour estimates provided by maintenance planning and other groups to
the radiation protection group with the actual work activity time requirements
Post-job (work activity) reviews
Assumptions and basis for the current annual collective exposure estimate, the
methodology for estimating work activity exposures, the intended dose outcome,
and the accuracy of dose rate and man-hour estimates
Method for adjusting exposure estimates, or re-planning work, when unexpected
changes in scope or emergent work were encountered
Exposure tracking system
- 15 -
Enclosure
Exposures of individuals from selected work groups
Records detailing the historical trends and current status of tracked plant source
terms and contingency plans for expected changes in the source term due to
changes in plant fuel performance issues or changes in plant primary chemistry
Declared pregnant workers during the current assessment period, monitoring
controls, and the exposure results
Self-assessments, audits, and special reports related to the ALARA program
since the last inspection
Resolution through the corrective action process of problems identified through
post-job reviews and post-outage ALARA report critiques
The inspector completed 11 of the required 15 samples and 5 of the optional samples as
defined in IP 71121.02-05.
4.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
.1
Data Submission Issue
a.
Inspection Scope
The inspectors performed a review of the data submitted by the licensee for the second
quarter of 2009 performance indicators for any obvious inconsistencies prior to its public
release in accordance with Inspection Manual Chapter 0608, Performance Indicator
Program.
This review was performed as part of the inspectors normal plant status activities and,
as such, did not constitute a separate inspection sample.
b.
Findings
No findings of significance were identified.
.2
Safety System Functional Failures
a.
Inspection Scope
The inspectors sampled licensee submittals for the Safety System Functional Failures
performance indicator for the period from the second quarter of 2008 through the second
quarter of 2009. To determine the accuracy of the performance indicator data reported
during those periods, performance indicator definitions and guidance contained in NEI
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5,
and NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73" definitions
and guidance were used. The inspectors reviewed the licensees operator narrative
logs, operability assessments, maintenance rule records, maintenance work orders,
- 16 -
Enclosure
issue reports, event reports and NRC Integrated Inspection reports for the period
beginning the second quarter of 2008 through the second quarter of 2009 to validate the
accuracy of the submittals. The inspectors also reviewed the licensees issue report
database to determine if any problems had been identified with the performance
indicator data collected or transmitted for this indicator and none were identified.
Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of one safety system functional failures sample as
defined in Inspection Procedure 71151-05.
b.
Findings
No findings of significance were identified.
.3
Mitigating Systems Performance Index - Emergency ac Power System
a.
Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance
Index (MSPI) - Emergency ac Power System performance for the period from the
second quarter of 2008 through the second quarter of 2009. To determine the accuracy
of the performance indicator data reported during those periods, performance indicator
definitions and guidance contained in NEI Document 99-02, Regulatory Assessment
Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the
licensees operator narrative logs, mitigating systems performance index derivation
reports, issue reports, event reports and NRC integrated inspection reports for the period
beginning the second quarter of 2008 through the second quarter of 2009 to validate the
accuracy of the submittals. The inspectors reviewed the mitigating systems performance
index component risk coefficient to determine if it had changed by more than 25 percent
in value since the previous inspection, and if so, that the change was in accordance with
applicable NEI guidance. The inspectors also reviewed the licensees issue report
database to determine if any problems had been identified with the performance
indicator data collected or transmitted for this indicator and none were identified.
Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of one mitigating systems performance index
emergency ac power system sample as defined in Inspection Procedure 71151-05.
b.
Findings
No findings of significance were identified.
.4
Mitigating Systems Performance Index - Cooling Water Systems
a.
Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance
Index - Cooling Water Systems performance for the period from the second quarter of
2008 through the second quarter of 2009. To determine the accuracy of the
performance indicator data reported during those periods, performance indicator
definitions and guidance contained in NEI Document 99-02, Regulatory Assessment
- 17 -
Enclosure
Performance Indicator Guideline, Revision 5, was used. The inspectors reviewed the
licensees operator narrative logs, issue reports, mitigating systems performance index
derivation reports, event reports and NRC integrated inspection reports for the period
beginning the second quarter of 2008 through the second quarter of 2009 to validate the
accuracy of the submittals. The inspectors reviewed the mitigating systems performance
index component risk coefficient to determine if it had changed by more than 25 percent
in value since the previous inspection, and if so, that the change was in accordance with
applicable NEI guidance. The inspectors also reviewed the licensees issue report
database to determine if any problems had been identified with the performance
indicator data collected or transmitted for this indicator and none were identified.
Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of one mitigating systems performance index
cooling water system sample as defined in Inspection Procedure 71151-05.
b.
Findings
No findings of significance were identified.
.16
Occupational Exposure Control Effectiveness (OR01)
a.
Inspection Scope
The inspector sampled licensee submittals for the Occupational Radiological
Occurrences performance indicator for the first quarter of 2009 through the third quarter
of 2009. To determine the accuracy of the performance indicator data reported during
those periods, performance indicator definitions and guidance contained in NEI
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5,
were used. The inspector reviewed the licensees assessment of the performance
indicator for occupational radiation safety to determine if indicator related data was
adequately assessed and reported. To assess the adequacy of the licensees
performance indicator data collection and analyses, the inspector discussed with
radiation protection staff, the scope and breadth of its data review, and the results of
those reviews. The inspector independently reviewed electronic dosimetry dose rate
and accumulated dose alarm and dose reports and the dose assignments for any
intakes that occurred during the time period reviewed to determine if there were
potentially unrecognized occurrences. The inspector also conducted walkdowns of
numerous locked high and very high radiation area entrances to determine the adequacy
of the controls in place for these areas.
These activities constitute completion of the occupational radiological occurrences
sample as defined in Inspection Procedure 71151-05.
b.
Findings
No findings of significance were identified.
- 18 -
Enclosure
.17
Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual
Radiological Effluent Occurrences (PR01)
a.
Inspection Scope
The inspector sampled licensee submittals for the Radiological Effluent Technical
Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences
performance indicator for the first quarter of 2009 through the third quarter of 2009. To
determine the accuracy of the performance indicator data reported during those periods,
performance indicator definitions and guidance contained in NEI Document 99-02,
Regulatory Assessment Performance Indicator Guideline, Revision 5, was used. The
inspector reviewed the licensees issue report database and selected individual reports
generated since this indicator was last reviewed to identify any potential occurrences
such as unmonitored, uncontrolled, or improperly calculated effluent releases that may
have impacted offsite dose. The inspector reviewed gaseous effluent summary data and
the results of associated offsite dose calculations for selected dates during the third
quarter of 2009 to determine if indicator results were accurately reported. The inspector
also reviewed the licensees methods for quantifying gaseous and liquid effluents and
determining effluent dose. Additionally, the inspector reviewed the licensees historical
10 CFR Part 50.75(g) file and selectively reviewed the licensees analysis for discharge
pathways resulting from a spill, leak, or unexpected liquid discharge focusing on those
incidents which occurred over the last few years.
These activities constitute completion of the radiological effluent technical
specifications/offsite dose calculation manual radiological effluent occurrences sample
as defined in Inspection Procedure 71151-05.
b.
Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical
Protection
.1
Routine Review of Identification and Resolution of Problems
a.
Inspection Scope
As part of the various baseline inspection procedures discussed in previous sections of
this report, the inspectors routinely reviewed issues during baseline inspection activities
and plant status reviews to verify that they were being entered into the licensees
corrective action program at an appropriate threshold, that adequate attention was being
given to timely corrective actions, and that adverse trends were identified and
addressed. The inspectors reviewed attributes that included: the complete and
accurate identification of the problem; the timely correction, commensurate with the
safety significance; the evaluation and disposition of performance issues, generic
implications, common causes, contributing factors, root causes, extent of condition
- 19 -
Enclosure
reviews, and previous occurrences reviews; and the classification, prioritization, focus,
and timeliness of corrective. Minor issues entered into the licensees corrective action
program because of the inspectors observations are included in the attached list of
documents reviewed.
These routine reviews for the identification and resolution of problems did not constitute
any additional inspection samples. Instead, by procedure, they were considered an
integral part of the inspections performed during the quarter and documented in
Section 1 of this report.
b.
Findings
No findings of significance were identified.
.2
Daily Corrective Action Program Reviews
a.
Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific
human performance issues for follow-up, the inspectors performed a daily screening of
items entered into the licensees corrective action program. The inspectors
accomplished this through review of the stations daily corrective action documents.
The inspectors performed these daily reviews as part of their daily plant status
monitoring activities and, as such, did not constitute any separate inspection samples.
b.
Findings
No findings of significance were identified.
.3
Semi-Annual Trend Review
a.
Inspection Scope
The inspectors performed a review of the licensees corrective action program and
associated documents to identify trends that could indicate the existence of a more
significant safety issue. The inspectors focused their review on repetitive equipment
issues, but also considered the results of daily corrective action item screening
discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human
performance results. The inspectors nominally considered the 6-month period of
January 2009 through July 2009, for a review of Operating Experience Smart Sample:
OpESS FY2009-02, A Negative trend and Recurring Events Involving feedwater
systems as it applies to the emergency feedwater system.
The inspectors also included issues documented outside the normal corrective action
program in major equipment problem lists, repetitive and/or rework maintenance lists,
departmental problem/challenges lists, system health reports, quality assurance
audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.
The inspectors compared and contrasted their results with the results contained in the
licensees corrective action program trending reports. Corrective actions associated with
- 20 -
Enclosure
- 21 -
Enclosure
a sample of the issues identified in the licensees trending reports were reviewed for
adequacy.
These activities constitute completion of one single semi-annual trend inspection sample
as defined in Inspection Procedure 71152-05.
b.
Findings
No findings of significance were identified.
4OA5 Other Activities
.1
Quarterly Resident Inspector Observations of Security Personnel and Activities
a.
Inspection Scope
During the inspection period, the inspectors performed observations of security force
personnel and activities to ensure that the activities were consistent with Waterford
Steam Electric Station security procedures and regulatory requirements relating to
nuclear plant security. These observations took place during both normal and off-normal
plant working hours.
These quarterly resident inspector observations of security force personnel and activities
did not constitute any additional inspection samples. Rather, they were considered an
integral part of the inspectors normal plant status review and inspection activities.
b.
Findings
No findings of significance were identified.
4OA6 Meetings
Exit Meeting Summary
On September 18, 2009, the team presented the inspection results to Mr. J. Kowalewski,
Vice President, Operations, and other members of his staff who acknowledged the findings.
The team confirmed that proprietary information was not provided or examined during the
inspection.
On October 1, 2009, the inspectors presented the inspection results to Mr. Joe Kowalewski, and
other members of the licensee staff. The licensee acknowledged the issues presented. The
inspector asked the licensee whether any materials examined during the inspection should be
considered proprietary. No proprietary information was identified.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
M. Adams, Supervisor, System Engineering
S. Anders, Manager, Plant Security
C. Arnone, Plant Manager
J. Brawley, ALARA Supervisor, Radiation Protection
B. Briner, Technical Specialist IV, Componet Engineering
K. Christian, Director, Nuclear Safety Assurance
K. Cook, Manager, Operations
L. Dauzat, Supervisor, Radiation Protection
D. Dufrene; Technician, Radiation Protection
C. Fugate, Assistant Manager, Operations
M. Haydel, Supervisor, Programs and Components
J. Kowalewski, Vice President of Operations
J. Lewis, Manager, Emergency Preparedness
B. Lindsey, Manager, Maintenance
M. Mason, Senior Licensing Specialist, Licensing
W. McKinney, Manager, Corrective Action and Assessments
C. Miller, Lead Supervisor, Radiation Protection
R. Murillo, Manager, Licensing
K. Nicholas, Director, Engineering
B. Piluti, Manager, Radiation Protection
J. Polluck, Engineer, Licensing
R. Putnam, Manager, Programs and Components
S. Ramzy; Specialist, Radiation Protection
J. Ridge, Manager, Quality Assurance
J. Solaski, Quality Assurance Auditor
J. Williams, Senior Licensing Specialist, Licensing
NRC Personnel
S. Anderson, General Engineer, HQ
T. Buchanan, Project Engineer, RIV
L. Carson II, Senior Health Physicist
M. Chambers, Resident Inspector, Cooper Nuclear Station
R. Egli, Branch Chief, Technical Training Center
R. Hickok, Senior Reactor Technology Instructor, Technical Training Center
P. Jayroe, Project Engineer, RIV
G. Replogle, Senior Project Engineer, RIV
A-1
Attachment
LIST OF ITEMS OPENED AND CLOSED
Opened and Closed 05000382/2009004-1
Failure to Follow Technical Specification Requirements for
Reactor Protective Instrumentation
LIST OF DOCUMENTS REVIEWED
Section 1RO1: Adverse Weather Protection
CONDITION REPORTS
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
OP-901-521
Sever Weather and Flooding
301
Section 1RO4: Equipment Alignment
CONDITION REPORTS
WORK ORDERS
190714
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
OP-903-045
Emergency Feedwater Flow Path Lineup Verification
5
OP-009-008
Safety Injection System
26
OP-002-005
Chemical and Volume Control
28
SD-CVC
Chemical and Volume Control System Description
6
SD-SI
Safety Injection System Description
6
A-2
Attachment
Section 1RO5: Fire Protection
CONDITION REPORTS
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
UNT-005-013
10
OP-009-004
Fire Protection
305
MM-004-424
Building Fire Hose Station Inspection and Hose
Replacement
10
MM-007-010
Fire Extinguisher Inspection and Extinguisher Replacement
302
Duties of a Fire Watch
14
Fire Protection Impairments
302
Appendix R/Fire Protection
Fire Protection Impairments
302
Pre-fire Plan Strategies, Development, And Revision
300
UNT-007-006
Housekeeping
301
Control of Combustibles
003
UNT-007-060
Control of Loose Items
302
UNT-005-013
010
Engineering Calculations F91-044
01
Engineering Calculations F91-019
0
Section 1R11: Licensed Operator Requalification Program
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
Simulator Scenario Number E-70
Simulator Scenario Number E-125
OP-901-201
Steam Generator Level Control System Malfunction
009
A-3
Attachment
OP-902-000
Standard Post Trip Actions
010
OP-902-008
Safety function Recovery Procedure
015
OP-901-110
Pressurizer Level Control Malfunction
005
OP-901-311
Loss of Train B Safety Bus
302
OP-901-102
300
OP-902-001
Reactor Trip Recovery
011
OP-902-002
Loss of Coolant Accident Recovery Procedure
012
Section 1R12: Maintenance Effectiveness
CONDITION REPORTS
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
Maintenance Rule
1
Industry Guideline for Monitoring the Effectiveness of
maintenance at Nuclear Power Plants
3
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
WORK ORDERS
51802942
52039753
0019397401
52192184
197692
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
OI-037-000
Operations Risk Management Guideline
300
On-Line Work Management Process
1
A-4
Attachment
W2.502
Configuration risk Management Program
000
OP-100-010
Equipment Out of Service
303
OP-903-107
Plant Protection System channel A & B & C & D
Functional Test
303
OP-903-030
Safety Injection Pump Operability Verification
18
OP-009-008
Safety Injection System
26
OP-006-003
125 VDC Electrical Distribution
301
ME-003-200
Station Battery Bank and Charger (Weekly)
301
ME-003-210
Station Battery Bank and Charger (Quarterly)
12
Section 1R15: Operability Evaluations
CONDITION REPORTS
WORK ORDERS
5180191
52038533
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
4
ME-003-200
Station Battery Bank and Charger (Weekly)
301
ME-003-210
Station Battery Bank and Charger (Quarterly)
12
OP-006-003
125 Vdc Electrical Distribution
301
OP-006-001
Plant Distribution System
305
MI-003-126
Core Protection Calculator Functional
14
SD-PPS
Plant Protection System Description
0
OP-903-107
Plant Protection System Channel A, B, C, D, Functional Test
303
Correct logarithmic power vs. RTP
1
A-5
Attachment
Section 1R18: Plant Modifications
CONDITION REPORTS
WORK ORDERS
203111
197692
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION /
DATE
4
EC NO: 706
Modification of containment relief valves
0
Implement EC 706
2/3/2007
Implement EC 15451
2/3/2007
ME-004-213
Battery Intercell Connections
14
16496
Section 1R19: Postmaintenance Testing
CONDITION REPORTS
WORK ORDERS
199029
51802942
52039753
0019397401
199977
188048
52040097
52038057
51523543
201698
52194563
197692
5180191
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
OP-903-030
Safety Injection Pump Operability Verification
15
OP-903-068
Emergency Diesel Generator Operability and Subgroup
Relay Operability Verification
303
OP-009-008
Safety Injection System
25
A-6
Attachment
Section 1R19: Postmaintenance Testing
CONDITION REPORTS
WORK ORDERS
199029
51802942
52039753
0019397401
199977
188048
52040097
52038057
51523543
201698
52194563
197692
5180191
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
OP-903-118
Primary Auxiliaries Quarterly IST Valve Tests
18
OP-903-037
Containment Cooling Fan Operability Verification
5
OP-903-119
Secondary Auxiliaries Quarterly IST Valve Tests
9
OP-903-120
Containment and Miscellaneous Systems Quarterly IST
Valve Tests
9
OP-903-003
Charging Pump Operability Check
301
ME-004-213
Battery Intercell Connections
14
OP-903-118
Primary Auxiliaries Quarterly IST Valve Tests
18
ME-007-002
15
SD-CC
Component Cooling Water and Auxiliary Component
Cooling Water System Description
7
STA-001-005
Leakage testing of Air and Nitrogen Accumulators for Safety
Related Valves
304
Section 1R22: Surveillance Testing
CONDITION REPORTS
CR-WR3-2009-4395
CR-WR3-2009-4466
A-7
Attachment
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
ME-003-318
G.E. Undervoltage Relay Model 121AV55C
303
OP-009-002
Emergency Diesel Generator Start Evaluation [Data Sheet]
310
OP-009-002
Diesel Generator Start Running Log
310
OP-903-068
Emergency Diesel Generator A Surveillance Test
OP-903-068
Emergency Diesel Generator and Subgroup Relay
Operability Verification - Train B
303
OP-903-030
Safety Injection Pump Operability Verification
18
OP-009-008
Safety Injection System
26
OP-903-107
Plant Protection System Channel B Functional Test
303
MI-003-126
Core Protection Calculator Functional
014
Section 1EP6: Drill Evaluation
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
Recognition and Classification of Emergency Conditions
22
Site Area Emergency
300
General Emergency
300
Scenario DEP 2007-02
Section 2OS2: ALARA Planning and Controls
PROCEDURES/DOCUMENTS
NUMBER
TITLE
REVISION
Radiological Control
0
Radiation Work Permits
4
Radiological Survey Documentation
2
ALARA Program
2
Job Coverage
6
EN-DIR-RP-002
Radiation Protection Performance Indicator
0
A-8
Attachment
AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES
NUMBER
TITLE
DATE
QA-14/15-2009-WF3-1
Radiation Protection/Radwaste Audit
Quality Oversight Observations
May 2008
RADIATION WORK PERMITS
RWP#
RWP DESCRIPTION
2008-0511
1R15 S/G Primary Side Eddy Current Testing Inspection and Repair
2008-0610
1R Scaffolding
2008-0631
1R15 Alloy 600 Mitigation Activities Pressurizer/Hot Legs (Weld Overlay)
2008-0702
Reactor Disassembly
2008-0705
Reactor Reassembly
CONDITION REPORTS
CR-WF3-2008-1699 CR-WF3-2008-1776
CR-WF3-2008-1793 CR-WF3-2008-1946
CR-WF3-2008-1989 CR-WF3-2008-2027
CR-WF3-2008-2347 CR-WF3-2008-4495
CR-WF3-2009-4959 CR-WF3-2009-4969
MISCELLANEOUS
TITLE
DATE
Waterford 3 Refuel Reactor Coolant System Dose Equivalent Iodine
September 10, 2009
Reactor Coolant System Cleanup Flow Chart
5-Year ALARA Plan
Refueling Outage 15 Report
Failed Fuel Shutdown Mitigation Plan
Section 4OA1: Performance Indicator Verification
PROCEDURES
NUMBER
TITLE
REVISION
Regulatory Assessment Performance Indicator Guideline
5
Performance Indicator Process
4
A-9
Attachment
A-10
Attachment
Section 4OA2: Identification and Resolution of Problems
CONDITION REPORTS
CR-WF3-2009-
WORK ORDERS
178225
51665138
PROCEDURES
NUMBER
TITLE
REVISION
EFW System Health Report 1st Quarter 2009
4/30/09