IR 05000458/2016002

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NRC Integrated Inspection Report 5000458/2016002 & 07200049/2016001
ML16211A189
Person / Time
Site: River Bend  Entergy icon.png
Issue date: 07/29/2016
From: Greg Warnick
NRC/RGN-IV/DRP/RPB-C
To: Maguire W
Entergy Operations
Greg Warnick
References
IR 2016001, IR 2016002
Download: ML16211A189 (49)


Text

July 29, 2016

SUBJECT:

RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2016002 AND 07200049/2016001

Dear Mr. Maguire:

On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station, Unit 1. On July 18, 2016, the NRC inspectors discussed the results of this inspection with you and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented three findings of very low safety significance (Green) in this report.

All of these findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violations or significance of these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the River Bend Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555 0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the River Bend Station.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Gregory G. Warnick, Chief Project Branch C Division of Reactor Projects

Docket Nos. 50-458,72-049 License Nos. NPF-47

Enclosure:

Inspection Report 05000458/2016002 and 07200049/2016001 w/ Attachments:

1) Supplemental Information 2) Request for Information for the O

REGION IV==

Docket:

05000458 and 07200049 License:

NPF-47 Report:

05000458/2016002 and 07200049/2016001 Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station Location:

5485 U.S. Highway 61N St. Francisville, LA 70775 Dates:

April 1 through June 30, 2016 Inspectors:

J. Sowa, Senior Resident Inspector B. Parks, Acting Resident Inspector F. Ramirez, Senior Resident Inspector M. Phalen, Senior Health Physicist P. Hernandez, Health Physicist L. Brookhart, Senior ISFSI Inspector, FCDB Approved By: G. Warnick, Chief Project Branch C Division of Reactor Projects

- 2 -

SUMMARY

IR 05000458/2016002, IR 07200049/2016001; 04/01/2016 - 06/30/2016; River Bend Station;

Fire Protection; Problem Identification and Resolution

The inspection activities described in this report were performed between April 1 and June 30, 2016, by the resident inspectors at River Bend Station and inspectors from the NRCs Region IV office and other NRC offices. Three findings of very low safety significance (Green)are documented in this report. All of these findings involved violations of NRC requirements.

The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using NRC Inspection Manual Chapter 0310, Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.

Cornerstone: Mitigating Systems

Green.

The inspectors identified a non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to follow station maintenance procedures related to the use of temporary power cables and storage of transient combustible materials in the auxiliary building. Specifically, the licensee installed energized networking equipment and an associated power cable within one foot of a safety-related cable tray. The station did not initially correct the problem, but later resolved the deficiencies by removing the networking equipment and power cable. The failure to initially correct the issue is documented as a violation in Section 4OA2 of this report. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2016-02398.

The licensees installation of energized networking equipment and an associated power cable within one foot of a safety-related cable tray was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it affected the protection against external factors attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, a fire resulting from this energized equipment would impact the availability, reliability, and capability of the low pressure core spray system, residual heat removal system, component cooling primary system, and reactor core isolation cooling system. The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings. Since the finding involved a failure to adequately implement fire prevention and administrative controls for transient combustibles, the inspectors dispositioned the finding using NRC Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process. In accordance with Manual Chapter 0609, Appendix F, Question 1.3.1.A, the inspectors determined that the finding was of very low safety significance (Green) because the reactor would be able to reach and maintain safe shutdown since the safe shutdown path was deemed independent of fire damage state scenarios for the given fire ignition source. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensees work management processes failed to plan, control, and execute the work activity that included installation of temporary equipment such that impacts on nuclear safety were properly evaluated and addressed [H.5]. (Section 1R05)

Green.

The inspectors identified a non-cited violation of Technical Specification 3.8.1, AC Sources - Operating, for the licensees failure to take required actions for an inoperable emergency diesel generator. Specifically, after classifying the Division I emergency diesel generator as inoperable on the basis of a nonconforming condition discovered during an extended maintenance outage, and after failing to either verify that the Division II emergency diesel generator was not inoperable due to common cause failure within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or conduct a surveillance run on the Division II emergency diesel generator within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, the licensee failed to enter Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, as required by Actions C.3.1, C.3.2, and G.1 of Technical Specification 3.8.1, respectively. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2016-03978. Corrective actions included the scheduling of training to ensure that operations personnel fully understand the technical specification requirements for common cause evaluation as they relate to adverse conditions on emergency diesel generators.

The failure to take required actions for an inoperable emergency diesel generator was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment reliability attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to follow technical specification requirements to ensure the availability, reliability, and capability of the operable emergency diesel generator directly affected the cornerstone objective. Using NRC Inspection Manual Chapter 0609,

Significance Determination Process, Appendix A, Exhibit 2 -- Mitigating Systems Screening Questions, the inspectors determined the finding to be of very low safety significance (Green) because the finding did not represent an actual loss of function of the Division II emergency diesel generator. The finding had a cross-cutting aspect in the area of human performance, consistent process, because the licensee failed to use a consistent, systematic approach to make decisions. Specifically, the licensee failed to review the required actions of the applicable technical specification so as to ensure that all of those actions would be properly carried out [H.13]. (Section 4OA2.2)

Green.

The inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, for the licensees failure to promptly identify and correct a condition adverse to quality. Specifically, after writing a condition report identifying energized networking equipment and an associated power cable that had been installed within one foot of a safety-related cable tray, the licensee closed the condition report without removing the networking equipment and power cable. The licensee entered this issue into their corrective action program as Condition Reports CR-RBS-2016-02398 and CR-RBS-2016-03152. Corrective actions included removing the networking equipment and power cable and conducting a performance management review of the actions involved with correcting the condition and closing the condition report.

The licensees failure to promptly identify and correct a condition adverse to quality was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it affected the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to correct a known deficient condition resulted in an extended period of vulnerability to a fire that could result from improperly installed energized equipment and challenge the availability, reliability, and capability of the low pressure core spray system, residual heat removal system, component cooling primary system, and reactor core isolation cooling system.

The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings. Since the finding involved a failure to adequately implement fire prevention and administrative controls for transient combustibles, the inspectors dispositioned the finding using NRC Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process. In accordance with Manual Chapter 0609, Appendix F, Question 1.3.1.A, the inspectors determined that the finding was of very low safety significance (Green) because the reactor would be able to reach and maintain safe shutdown since the safe shutdown path was deemed independent of fire damage state scenarios for the given fire ignition source. The finding had a cross-cutting aspect in the area of human performance, teamwork, because the licensee failed to properly communicate expectations to individuals performing work during the course of implementing corrective actions [H.4]. (Section 4OA2.3)

PLANT STATUS

River Bend Station (RBS) began the inspection period at 100 percent reactor thermal power. It departed from full power as follows:

  • On April 7, 2016, the station reduced power to 67 percent to conduct suppression testing to identify and suppress a leaking fuel assembly. The station returned the unit to 100 percent power on April 9, 2016.
  • On June 11, 2016, the station conducted a shutdown in order to diagnose and replace leaking fuel assemblies. The station returned the unit to 100 percent power on June 28, 2016.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Summer Readiness for Offsite and Alternate AC Power Systems

a. Inspection Scope

On June 6, 2016, the inspectors completed an inspection of the stations offsite and alternate-ac power systems. The inspectors inspected the material condition of these systems, including transformers and other switchyard equipment, to verify that plant features and procedures were appropriate for operation and continued availability of offsite and alternate-ac power systems. The inspectors reviewed outstanding work orders and open condition reports (CRs) for these systems. The inspectors walked down the switchyard to observe the material condition of equipment providing offsite power sources. The inspectors verified that the licensees procedures included appropriate measures to monitor and maintain availability and reliability of the offsite and alternate-ac power systems.

These activities constitute one sample of summer readiness of offsite and alternate-ac power systems, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

.2 Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

On June 3, 2016, the inspectors completed an inspection of the stations readiness for impending adverse weather conditions. The inspectors reviewed plant design features, the licensees procedures to respond to tornadoes and high winds, and the licensees planned implementation of these procedures. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant.

These activities constitute one sample of readiness for impending adverse weather conditions, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constitute three partial system walkdown samples, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on six plant areas important to safety:

  • April 22, 2016, auxiliary building, low pressure core spray pump room, fire area AB-6/Z-2
  • April 25, 2016, control building, Division II control building chiller room, fire area C-13E
  • May 19, 2016, auxiliary building, standby gas treatment B room, fire area AB-13
  • May 27, 2016, diesel generator building, diesel generator A room, fire area DG-6/Z-1
  • May 27, 2016, reactor building, hydraulic control unit area east, fire area RC-3/Z-3
  • May 27, 2016, reactor building, hydraulic control unit area west, fire area RC-4/Z-3

For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constitute six quarterly inspection samples, as defined in Inspection Procedure 71111.05.

b. Findings

Introduction.

The inspectors identified a Green, non-cited violation of Technical Specification (TS) 5.4.1.a, for the licensees failure to follow station maintenance procedures related to the use of temporary power cables and storage of transient combustible materials in the auxiliary building. Specifically, the licensee installed energized networking equipment and an associated power cable within one foot of a safety-related cable tray. The station did not initially correct the problem, but later resolved the deficiencies by removing the networking equipment and power cable. The failure to initially correct the issue is documented as a violation in Section 4OA2 of this report. The licensee entered this issue into their corrective action program (CAP) as Condition Report CR-RBS-2016-02398.

Description.

On March 18, 2016, the inspectors discovered energized electronic networking equipment secured with tie wraps to safety-related cable tray 1TX808R in the low pressure core spray pump hatch room on the 95-foot elevation of the auxiliary building (fire area AB-6, zone 2). The inspectors also observed a temporary power cable supplying power to the networking equipment situated inside of safety-related cable tray 1TX808R. The inspectors evaluated the cables in the cable tray and determined that 55 Division I safety-related cables were routed through this tray. These cables supply power to components associated with the low pressure core spray system, residual heat removal system, component cooling primary system, reactor core isolation cooling system, and leak detection system. Of these 55 cables, 25 supply power to components designated as necessary for safe shutdown of the plant. These components would be adversely affected in the event of a fire from the energized equipment. The inspectors immediately notified control room personnel. The licensee wrote Condition Report CR-RBS-2016-02398 and ultimately corrected the condition by removing the networking equipment and power cable.

The inspectors reviewed station Procedure ADM-0073, Temporary Services and Equipment, Revision 307. Procedure ADM-0073, Step 8.2.3, requires temporary electrical cords less than 240 volts to have a minimum clearance of one foot from permanent cables and conduits. Additionally, the inspectors reviewed Procedure EN-DC-161, Control of Combustibles, Revision 13, and noted that Step 5.2[4] stated:

Transient combustible materials should be located in designated storage areas or arranged so as to minimize the fire hazard to cable trays and plant equipment. Do NOT place combustible materials directly under or over cable trays.

River Bend Station Updated Safety Analysis Report, Section 9A.2.5.1.7.2, states the major contributor to fire severity for fire area AB-6 is cable insulation. The networking equipment and energized power cable were secured to and in direct contact with the insulated safety-related cables in cable tray 1TX808R. The equipment was installed on February 20, 2015.

Analysis.

The licensees installation of energized networking equipment and an associated power cable within one foot of a safety-related cable tray was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it affected the protection against external factors attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, a fire resulting from this energized equipment would impact the availability, reliability, and capability of the low pressure core spray system, residual heat removal system, component cooling primary system, and reactor core isolation cooling system.

The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings. Since the finding involved a failure to adequately implement fire prevention and administrative controls for transient combustibles, the inspectors dispositioned the finding using Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process. In accordance with Manual Chapter 0609, Appendix F, Question 1.3.1.A, the inspectors determined that the finding was of very low safety significance (Green) because the reactor would be able to reach and maintain safe shutdown since the safe shutdown path was deemed independent of fire damage state scenarios for the given fire ignition source. The finding had a cross-cutting aspect in the area of human performance, work management, because the licensees work management processes failed to plan, control, and execute the work activity that included installation of temporary equipment such that impacts on nuclear safety were properly evaluated and addressed [H.5].

Enforcement.

Technical Specification 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.a of Appendix A to Regulatory Guide 1.33, Revision 2, requires procedures for performing maintenance. The licensee established Procedure ADM-0073, Temporary Services and Equipment, Revision 307, to meet the Regulatory Guide 1.33 requirement. Procedure ADM-0073, Temporary Services and Equipment, Revision 307, Step 8.2.3, requires temporary electrical cables less than 240 volts to have a minimum clearance of one foot from permanent cables and conduits. Contrary to the above, from February 20, 2015, to April 25, 2016, the licensee did not implement the maintenance procedure requirement that temporary electrical cables less than 240 volts have a minimum clearance of one foot from permanent cables and conduits. Specifically, the licensee mounted energized networking equipment and a temporary power cable directly to safety-related cable tray 1TX808R. As a result, the licensee introduced an ignition source that increased the frequency of a fire that could adversely impact safety-related equipment. The licensee entered this condition into their CAP as Condition Report CR-RBS-2016-02398. The licensee restored compliance by removing the networking equipment and temporary power cable. Because this finding is of very low safety significance and was entered into the licensees CAP as Condition Report CR-RBS-2016-03152, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the Enforcement Policy: NCV 05000458/2016002-01, Failure to Follow Station Guidance on Use of Temporary Power Cables and Control of Transient Combustibles.

.2 Annual Inspection

a. Inspection Scope

This evaluation included observation of an unannounced fire drill for training on April 27, 2016.

During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigades use of turnout gear and fire-fighting equipment, and the effectiveness of the fire brigades team operation. The inspectors also reviewed whether the licensees fire brigade met NRC requirements for training, dedicated size and membership, and equipment.

These activities constitute one annual inspection sample, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On May 4, 2016, the inspectors observed a portion of an annual requalification test for licensed operators. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities.

These activities constitute completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

On April 7, 2016, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity due to conducting suppression testing.

In addition, the inspectors assessed the operators adherence to plant procedures, including the conduct of operations procedures and other operations department policies.

These activities constitute completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed two instances of degraded performance or condition of safety-related structures, systems, and components (SSCs):

The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constitute completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed five risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:

  • April 5, 2016, green risk associated with the inability to remotely operate breaker YCB-OCB-20610, Division I reserve station service isolation from the south offsite power bus
  • April 18, 2016, yellow risk condition while Division II standby service water was out of service for maintenance concurrent with Division II residual heat removal system out of service
  • April 27, 2016, yellow risk condition due to upgrades at Fancy Point switchyard with station blackout diesel generator out of service for maintenance

The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.

These activities constitute completion of five maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed four operability determinations that the licensee performed for degraded or nonconforming SSCs:

The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.

These activities constitute completion of four operability and functionality review samples, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

On June 30, 2016, the inspectors reviewed a temporary modification to replace the variseals associated with the feedwater regulating valves with a replacement O-ring.

The inspectors verified that the licensee had installed this temporary modification in accordance with technically adequate design documents. The inspectors verified that this modification did not adversely impact the operability or availability of affected SSCs.

The inspectors reviewed design documentation and plant procedures affected by the modification to verify the licensee maintained configuration control.

These activities constitute completion of one sample of temporary modifications, as defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed six post-maintenance testing activities that affected risk-significant SSCs:

  • April 8, 2016, work order (WO) 00440426, Division I Alternate Depressurization System (ADS) Trip Unit B21-ESN670E Repair, following spurious tripping and resetting of the trip unit
  • May 19, 2016, WO 00445871, Post-Maintenance Testing after Installation of TMOD 64705 for EJS-SWG2B-ACB072, following implementation of temporary modification to standby gas treatment B supply breaker EJS-SWG2B-ACB072
  • May 23, 2016, WO 00445913-07, Post-Maintenance Testing after Installation of TMOD 64709 for EJS-SWG2A-ACB032, following implementation of temporary modification to standby gas treatment A supply breaker EJS-SWG2A-ACB032

The inspectors reviewed licensing-and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constitute completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

During the stations maintenance outage that concluded on June 25, 2016, the inspectors evaluated the licensees outage activities. The inspectors verified that the licensee considered risk in developing and implementing the outage plan, appropriately managed personnel fatigue, and developed mitigation strategies for losses of key safety functions. This verification included the following:

  • Review of the licensees outage plan prior to the outage
  • Review and verification of the licensees fatigue management activities
  • Monitoring of shutdown and cooldown activities
  • Verification that the licensee maintained defense-in-depth during outage activities
  • Observation and review of fuel handling activities
  • Monitoring of heatup and startup activities These activities constitute completion of one outage activities sample, as defined in Inspection Procedure 71111.20.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed five risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:

In-service test:

  • April 29, 2016, STP-209-6310, RCIC Quarterly Pump and Valve Operability Test, performed on April 15, 2016

Containment isolation valve surveillance test:

  • June 2, 2016, STP-057-3805, CRD Containment Control Rod Drive Removal Hatch Leak Rate Test, performed on February 23, 2016

Other surveillance tests:

  • May 5, 2016, STP-309-0206, Division I Diesel Generator 184 Operability Test, performed on May 2, 2016
  • June 1, 2016, STP-203-1702, E22-S001 Battery Performance Discharge Test, performed on May 26, 2016
  • June 1, 2016, STP-051-4610, RPS/RHR - Reactor Vessel Steam Dome Pressure-High Channel Functional Test, performed on May 26, 2016

The inspectors verified that these tests met TS requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constitute completion of five surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

Training Evolution Observation

a. Inspection Scope

On April 26, 2016, the inspectors observed simulator-based licensed operator requalification training that included implementation of the licensees emergency plan.

The inspectors verified that the licensees emergency classifications, offsite notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the evaluators and entered into the CAP for resolution.

These activities constitute completion of one training observation sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls

a. Inspection Scope

The inspectors evaluated the licensees performance in assessing the radiological hazards in the workplace associated with licensed activities. The inspectors assessed the licensees implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, performed independent radiation dose rate measurements, and observed postings and physical controls. The inspectors reviewed licensee performance in the following areas:

  • Radiological hazard assessment, including a review of the plants radiological source terms and associated radiological hazards. The inspectors also reviewed the licensees radiological survey program to determine whether radiological hazards were properly identified for routine and non-routine activities and assessed for changes in plant operations.
  • Instructions to workers including radiation work permit requirements and restrictions, actions for electronic dosimeter alarms, changing radiological condition, and radioactive material container labeling.
  • Contamination and radioactive material control, including release of potentially contaminated material from the radiologically controlled area, radiological survey performance, radiation instrument sensitivities, material control and release criteria, and control and accountability of sealed radioactive sources.
  • Radiological hazards control and work coverage. During walkdowns of the facility and job performance observations, the inspectors evaluated ambient radiological conditions, radiological postings, adequacy of radiological controls, radiation protection job coverage, and contamination controls. The inspectors also evaluated dosimetry selection and placement as well as the use of dosimetry in areas with significant dose rate gradients. The inspectors examined the licensees controls for items stored in the spent fuel pool and evaluated airborne radioactivity controls and monitoring.
  • Radiation worker performance and radiation protection technician proficiency with respect to radiation protection work requirements. The inspectors determined if workers were aware of significant radiological conditions in their workplace, radiation work permit controls/limits in place, and electronic dosimeter dose and dose rate set points. The inspectors observed radiation protection technician job performance, including the performance of radiation surveys.
  • Problem identification and resolution for radiological hazard assessment and exposure controls. The inspectors reviewed audits, self-assessments, and CAP documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the seven required samples of radiological hazard assessment and exposure control program, as defined in Inspection Procedure 71124.01.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

a. Inspection Scope

The inspectors evaluated whether the licensee controlled in-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, and reviewed licensee performance in the following areas:

  • Engineering controls, including the use of permanent and temporary ventilation systems to control airborne radioactivity. The inspectors evaluated installed ventilation systems, including review of procedural guidance, verification the systems were used during high-risk activities, and verification of airflow capacity, flow path, and filter/charcoal unit efficiencies. The inspectors also reviewed the use of temporary ventilation systems used to support work in contaminated areas such as high efficiency particulate air (HEPA)/charcoal negative pressure units.

Additionally, the inspectors evaluated the licensees airborne monitoring protocols, including verification that alarms and set points were appropriate.

  • Use of respiratory protection devices, including an evaluation of the licensees respiratory protection program for use, storage, maintenance, and quality assurance of National Institute for Occupational Safety and Health (NIOSH)certified equipment, air quality and quantity for supplied-air devices and self-contained breathing apparatus (SCBA) bottles, qualification and training of personnel, and user performance.
  • Self-contained breathing apparatus for emergency use, including the licensees capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions, hydrostatic testing of SCBA bottles, status of SCBA staged and ready for use in the plant including vision correction, mask sizes, etc., SCBA surveillance and maintenance records, and personnel qualification, training, and readiness.
  • Problem identification and resolution for airborne radioactivity control and mitigation. The inspectors reviewed audits, self-assessments, and corrective action documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the four required samples of in-plant airborne radioactivity control and mitigation program, as defined in Inspection Procedure 71124.03.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Safety System Functional Failures (MS05)

a. Inspection Scope

For the period of April 2015 through March 2016, the inspectors reviewed licensee event reports (LERs), maintenance rule evaluations, and other records that could indicate whether safety system functional failures had occurred. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, and NUREG-1022, Event Reporting Guidelines: 10 CFR 50.72 and 50.73, Revision 3, to determine the accuracy of the data reported.

These activities constitute verification of the safety system functional failures performance indicator for Unit 1, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index: Emergency AC Power Systems (MS06)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of April 2015 through March 2016 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for emergency ac power systems for Unit 1, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of April 2015 through March 2016 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the mitigating system performance index for high pressure injection systems for Unit 1, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.4 Occupational Exposure Control Effectiveness (OR01)

a. Inspection Scope

The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period of January 2015 through March 2016. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than 100 millirem. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the occupational exposure control effectiveness performance indicator, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.5 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual

(ODCM) Radiological Effluent Occurrences (PR01)

a. Inspection Scope

The inspectors verified that there were no liquid or gaseous effluent releases that occurred during the period of January 2015 through March 2016. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constitute verification of the radiological effluent technical specifications (RETS)/offsite dose calculation manual (ODCM) radiological effluent occurrences performance indicator, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees CAP and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the CAP for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Semiannual Trend Review

a. Inspection Scope

The inspectors reviewed the licensees CAP, performance indicators, system health reports, and other documentation to identify trends that might indicate the existence of a more significant safety issue. To verify that the licensee was taking corrective actions to address adverse trends that might indicate the existence of a more significant safety issue, the inspectors reviewed CAP documentation associated with the following adverse trend:

  • From January 1, 2015, to December 31, 2015, the licensee experienced an increase in consequential events driven by inadequate procedure adherence.

This adverse trend continued through the second quarter of 2016.

These activities constitute completion of one semiannual trend review sample, as defined in Inspection Procedure 71152.

b.

Observations and Assessments The inspectors review produced the following observations and assessments:

  • The inspectors observed that the negative trend in procedure adherence continued into the 6-month period from January 1, 2016, to June 30, 2016.

Specifically, three instances of an inadequate procedure adherence that resulted in a consequential event were observed during the period.

o January 10, 2016: While installing a jumper to bypass the 135 psig isolations for the residual heat removal system, operations personnel failed to follow procedure and use a jumper with a retractable sheath.

Operations personnel subsequently caused a ground that led to a loss of shutdown cooling (CR-RBS-2016-00210). The finding associated with this performance deficiency is discussed in Section 2.11.a of Special Inspection Report 0500458/2016009 (ML16133A174).

o January 29, 2016: During testing of relaying associated with the offsite power line to Division I offsite power, an unanticipated relay actuation occurred resulting in a loss of Division I offsite power and an actuation of the Division I emergency diesel generator. The actuation was determined to be due, in part, to a failure to appropriately use required procedures and drawings during the maintenance (CR-RBS-2016-01027). This event is described in Licensee Event Report 2016-004.

o May 5, 2016: After classifying the Division I emergency diesel generator as inoperable on the basis of two potentially degraded conditions and one potentially nonconforming condition, the licensee failed to follow the TS requirement to either verify that similar conditions did not exist on the Division II emergency diesel generator or conduct a surveillance run of the Division II emergency diesel generator (CR-RBS-2016-03978).

c. Findings

Introduction.

The inspectors identified a Green, non-cited violation of TS 3.8.1, AC Sources - Operating, for the licensees failure to take required actions for an inoperable emergency diesel generator (EDG). Specifically, after classifying the Division I EDG as inoperable on the basis of a nonconforming condition discovered during an extended maintenance outage, and after failing to either verify that the Division II EDG was not inoperable due to common cause failure within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or conduct a surveillance run on the Division II EDG within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, the licensee failed to enter Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, as required by Actions C.3.1, C.3.2, and G.1 of TS 3.8.1, respectively. The licensee entered this issue into their CAP as Condition Report CR-RBS-2016-03978.

Description.

On May 5, 2016, with the Division I EDG out of service for an extended maintenance overhaul, the licensee attempted to conduct a scheduled 3-year replacement of the rubber insert on the Division I EDGs governor drive coupling assembly. During attempted installation of the new insert, the licensee discovered that the coupling gap on the assembly, which is the space that the insert fits into, was out of specification. Specifically, the coupling gap was measured to be five-eighths of an inch in length, in comparison with the vendor manual requirement of 1 inch. At that gap length, contortion of the rubber insert was necessary to fit into the reduced space.

At 10:18 p.m. on May 5, 2016, the licensee entered the nonconforming condition associated with the incorrect gap length into the CAP as Condition Report CR-RBS-2016-03516. Approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> later, at 2:01 a.m. the next day, the shift manager approved the control room supervisors determination that the condition rendered the Division I EDG inoperable.

On the evening of May 6, 2016, after discussions with the vendor, the licensee realized that the coupling assembly had been installed incorrectly, with its upper component oriented upside down. When the upper component was reoriented to a correct positioning, the coupling gap increased to 1 inch, consistent with the vendor manual requirement. The licensee was then able to smoothly install the rubber insert into the gap as designed.

The rubber insert joins the upper and lower ends of the governor drive together. If it were to fail, the governor would lose the connection through which it measures engine speed, and therefore the EDG would lose speed control. For this reason, the incorrect installation represented a nonconforming condition with the potential to render the Division I EDG inoperable. Step 5.3.1 of Procedure EN-OP-104, Operability Determination Process, Revision 10, requires the licensee to evaluate the impact of the nonconforming condition on the specified safety function of the diesel. However, no such evaluation was conducted. Instead, the control room supervisor classified the condition as inoperable without an evaluation since the EDG was already inoperable for the maintenance overhaul.

When a nonconforming condition renders a diesel generator inoperable, Actions C.3.1 and C.3.2 of TS 3.8.1 require the licensee to determine that the other operable EDGs are not inoperable due to common cause failure, or demonstrate the operability of the other EDGs by performing a surveillance run in accordance with surveillance requirement (SR) 3.8.1.2 within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. If those actions are not completed in the required time frame, TS 3.8.1, Action G.1, requires the licensee to enter Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

On May 9, 2016, after reviewing the condition report that documented the nonconforming condition and finding no evidence that a common cause evaluation or a surveillance run had been conducted in accordance with TS requirements, inspectors brought the issue to the attention of the licensee. After looking into the issue, the licensee confirmed that no common cause evaluation or surveillance run on the Division II EDG had been conducted, contrary to TS requirements. At that point, greater than 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> had passed since the discovery of the condition and the declaration of inoperability, and therefore the licensee was required to be in Mode 3.

After conferring with the system engineer, the shift manager concluded that the prior crews declaration of inoperability was overly conservative, and that the nonconforming condition, on its own, did not render the EDG inoperable. The shift manager therefore determined that Actions C.3.1, C.3.2, and G.1 of TS 3.8.1 did not apply.

At the time that the shift manager reached this conclusion, the engineering evaluation necessary to establish a reasonable expectation that the nonconforming EDG was operable, i.e., capable of performing its specified safety function, had not yet been completed. The licensee did not yet have a full understanding of the functions of the governor coupling, or of the impact that installing the rubber insert incorrectly, in a contorted fashion, would have on those functions, particularly in a scenario in which the EDG is called upon to run for seven continuous days at the end of a preventative maintenance cycle, when the insert will have experienced maximum wear and tear.

Therefore, the licensee did not have an appropriate basis for nonconservatively reversing the prior crews declaration and calling the nonconforming EDG operable.

The next day, the licensee completed an engineering evaluation of the condition, which was subsequently revised to address the inspectors questions. The licensee was ultimately able to demonstrate that the nonconforming EDG would have been able to perform its specified safety function across the spectrum of its design basis.

Additionally, in the weeks following the discovery of the nonconforming condition, the licensee inspected the rubber insert installation on the other EDG (Division II), and found it to be conforming.

To assess the extent of the performance deficiency, inspectors reviewed CRs from past EDG outages. Inspectors identified eight additional cases dating back to 2013 in which the licensee declared an already-inoperable EDG inoperable on the basis of a newly-identified adverse condition, without conducting a common cause evaluation of the condition or demonstrating the operability of the other EDGs in a surveillance run, as required by TS. In each of these cases, inspectors noted that there was a reasonable basis for expecting that the EDG would be capable of performing its specified safety function in the presence of the adverse condition, and therefore if an evaluation of the condition had been conducted in accordance with the operability determination procedure, the EDG would have been determined to be operable. Nonetheless, in each case, the licensee declared the EDG inoperable, without carrying out the required TS actions.

Analysis.

The failure to take required actions for an inoperable EDG was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment reliability attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to follow technical specification requirements to ensure the availability, reliability, and capability of the operable emergency diesel generator directly affected the cornerstone objective. Using NRC Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Exhibit 2 -- Mitigating Systems Screening Questions, the inspectors determined the finding to be of very low safety significance (Green) because the finding did not represent an actual loss of function of the Division II EDG. The finding had a cross-cutting aspect in the area of human performance, consistent process, because the licensee failed to use a consistent, systematic approach to make decisions. Specifically, the licensee failed to review the required actions of the applicable TS so as to ensure that all of those actions would be properly carried out [H.13].

Enforcement.

Technical Specification 3.8.1 requires, in part, that three diesel generators be operable in Modes 1, 2, and 3. For the condition of one EDG inoperable, Action C.3.1 and C.3.2 of TS 3.8.1 require the license to either determine that the operable EDG is not inoperable due to common cause failure within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, or perform SR 3.8.1.2 on the operable EDG within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. If these actions are not taken, Action G.1 of TS 3.8.1 requires the licensee to be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to the above, from May 7, 2016, to May 9, 2016, after declaring one EDG inoperable on the basis of one potentially nonconforming condition and two potentially degraded conditions, and after failing to either determine that the operable EDG was not inoperable due to common cause failure within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, or perform SR 3.8.1.2 on the operable EDG within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, the licensee failed to place the unit in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The licensee restored compliance by demonstrating that the nonconforming condition was insufficient to render the Division I EDG inoperable. Because this finding is of very low safety significance and was entered into the licensees CAP as Condition Report CR-RBS-2015-03978, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the Enforcement Policy: NCV 05000458/2016002-02, Failure to Conduct Common Cause Failure Evaluation in Response to Inoperable Emergency Diesel Generator.

.3 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors selected one issue for an in-depth follow-up:

  • On March 18, 2016, the inspectors discovered energized electronic networking equipment secured with tie wraps to safety-related cable tray 1TX808R in the low pressure core spray pump hatch room on the 95-foot elevation of the auxiliary building. The condition report was closed on March 29, 2016. The closure description stated that the condition report was closed because the condition was corrected. On April 22, 2016, the inspectors observed that energized networking equipment and a temporary power cable were still present in cable tray 1TX808R.

These activities constitute completion of one annual follow-up sample, as defined in Inspection Procedure 71152.

b. Findings

Introduction.

The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the licensees failure to promptly identify and correct a condition adverse to quality. Specifically, after writing a condition report identifying energized networking equipment and an associated power cable that had been installed within one foot of a safety-related cable tray, the licensee closed the condition report without removing the networking equipment and power cable. The licensee entered this issue into their CAP as CRs CR-RBS-2016-02398 and CR-RBS-2016-03152.

Description.

On March 18, 2016, the inspectors discovered energized electronic networking equipment secured with tie wraps to safety-related cable tray 1TX808R in the low pressure core spray pump hatch room on the 95-foot elevation of the auxiliary building (fire area AB-6, zone 2). This performance deficiency and associated finding are discussed in Section 1R05 of this report. The inspectors notified control room personnel. The licensee wrote Condition Report CR-RBS-2016-02355 to capture an aggregation of several observations noted by the inspectors on a plant tour that was performed on March 18, 2016. The licensee generated individual CRs for each of these observations on March 23, 2016. The licensee wrote Condition Report CR-RBS-2016-02398 to document the issue with the energized electronic networking equipment and power cable. This condition report was designated as an adverse condition. The condition report was closed on March 29, 2016. The closure description stated that the condition report was closed because the condition was corrected. On April 22, 2016, the inspectors observed that energized networking equipment and a temporary power cable were still present in cable tray 1TX808R despite the statement in Condition Report CR-RBS-2016-02398 that the condition had been corrected. The inspectors presented this information to operations department management, and the licensee wrote Condition Report CR-RBS-2016-03152 and corrected the condition by removing the networking equipment and power cable. Operations management indicated to the inspectors that Condition Report CR-RBS-2016-02398 was initially coded as closed after an operator removed equipment from cable tray 1TX808R different than the equipment identified by the inspectors and identified in CR-RBS-2016-02398.

Analysis.

The licensees failure to promptly identify and correct a condition adverse to quality was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it affected the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to correct a known deficient condition resulted in an extended period of vulnerability to a fire that could result from improperly installed energized equipment and challenge the availability, reliability, and capability of the low pressure core spray system, residual heat removal system, component cooling primary system, and reactor core isolation cooling system.

The inspectors performed the initial significance determination using NRC Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings. Since the finding involved a failure to adequately implement fire prevention and administrative controls for transient combustibles, the inspectors dispositioned the finding using NRC Inspection Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process. In accordance with Manual Chapter 0609, Appendix F, Question 1.3.1.A, the inspectors determined that the finding was of very low safety significance (Green) because the reactor would be able to reach and maintain safe shutdown since the safe shutdown path was deemed independent of fire damage state scenarios for the given fire ignition source. The finding had a cross-cutting aspect in the area of human performance, teamwork, because the licensee failed to properly communicate expectations to individuals performing work during the course of implementing corrective actions [H.4].

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to the above, between March 23, 2016, and April 25, 2016, the licensee failed to establish measures to assure that a condition adverse to quality was promptly identified and corrected. Specifically, the licensee failed to remove improperly stowed transient combustibles when notified by the inspectors. The licensee addressed this deficiency by removing the networking equipment and power cable and conducting a performance management review of the actions involved with correcting the condition and closing the condition report. Because this finding is of very low significance and was entered into the licensees CAP as Condition Report CR-RBS-2015-03152, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy: NCV 05000458/2016002-03, Failure to Identify and Correct Improperly Stowed Transient Combustibles.

4OA3 Follow-up of Events and Notices of Enforcement Discretion

.1 (Closed) Licensee Event Report (LER) 05000458/2015-009-01, Automatic Reactor

Scram Due to Partial Loss of Offsite Power Caused by Fault in Local 230kV Switchyard

This LER described additional, amplifying information to that contained in LER 2015-009-00, issued on January 26, 2016. The original LER described an automatic reactor scram from 100 percent power that occurred due to a partial loss of offsite power originating from a fault in the 230kV switchyard. This revision to the original LER provides additional information on the cause of the switchyard fault, which was determined to be an animal induced fault. The original LER was reviewed during a special inspection and was closed in NRC Inspection Report 05000458/2016009. The results of the review and the associated finding are discussed in Section 4OA3 of the special inspection report (ML16133A174). LER 05000458/2015-009-01 is closed.

These activities constitute completion of one event follow-up sample, as defined in Inspection Procedure 71153.

.2 (Closed) Unresolved Item (URI) 07200049/2012001-01, Fuel Assemblies Minimum

Enrichment is Not Bounded by Offsite Dose Calculation Required by 10 CFR 72.104 During the routine Independent Spent Fuel Storage Installation (ISFSI) inspection conducted on September 25-27, 2012, a URI was identified and documented in routine ISFSI NRC Inspection Report 05000458/2012011 and 07200049/2012001 (ML12299A101). Title 10 of Code of Federal Regulations (CFR) 72.212 (b)(5)(iii)requires general licensees to perform a written evaluation that demonstrates the radiological dose beyond the licensees controlled area boundary will not exceed 25 millirem a year as required by 10 CFR 72.104. During a review of RBSs 10 CFR 72.104 calculation in the Holtec HI-2043196 Report, NRC inspectors identified that conservative assumptions may not have been used. The Holtec Report, Section 4, Assumptions, and the computer files attached used 4 percent enrichment as the design basis fuel in the calculations. However, RBS had loaded several casks with enrichments below this value, such as Cask #8 where all 68 fuel assemblies were below 2.49 percent enrichment and Cask #16 with spent fuel assemblies as low as 2.231 percent enrichment. As fuel enrichments decrease, the dose from the cask increases for the same burnup. This is due to the fact that as the initial enrichment decreases, the fuel is exposed to a larger neutron fluence to achieve the same burnup. The larger neutron fluence generates larger actinide content which results in a larger neutron source term and secondary gamma source term as illustrated in NUREG/CR-6716, Recommendations on Fuel Parameters for Standard Technical Specifications for Spent Fuel Storage Casks. The NRC inspectors opened a URI because it was unclear if the licensees calculation, as required by 10 CFR 72.212 (b)(5)(iii), bounded all the fuel that had been placed at the ISFSI.

River Bend Station opened a condition report, CR-RBS-2012-06153, to track the URI and re-evaluate their calculation. The Holtec HI-2043196 Report, Revision 1, was created to analyze the bounding source terms of the currently loaded casks to determine if the licensees calculation remained bounded. The analysis also reviewed the licensees remaining fuel inventory that was in the spent fuel pool to ensure future loadings would also be bounded by the calculation. The Holtec Report concluded that radiation source terms for all fuel at RBS was bounded by the analyzed source terms from the original report. The original calculation utilized higher burnups and lower cooling times which presented a conservative calculation even though it utilized an assumed higher enrichment value. The inspectors concluded the licensee had performed adequate corrective actions to address the URI and demonstrated that their calculation conservatively met the 10 CFR 72.212 (b)(5)(iii) and 10 CFR 72.104 requirements.

No additional deficiencies were identified during review of this URI.

URI 07200049/2012001-01 is closed.

4OA5

OTHER ACTIVITIES

Operation of an Independent Spent Fuel Storage Facility at Operating Plants (60855.1)

a. Inspection Scope

A routine ISFSI inspection was conducted at the RBS on May 10-12, 2016, by Region IV Division of Nuclear Material Safety inspectors. The inspectors observed and evaluated select licensee loading, processing, and heavy load procedures associated with the licensees ISFSI program. Inspectors performed a review of the dry fuel storage records for the one canister that had been loaded at the ISFSI since the last NRC ISFSI inspection (August 2014). The canister contents were reviewed to verify that the licensee was loading fuel in accordance with the TS for approved contents. Additionally, contents of three previously loaded casks were also reviewed to verify document retrievability. Documents reviewed included multi-purpose canister (MPC) loading maps and fuel assembly specific information such as, identification, decay heat, cooling time, average U-235 enrichment, burnup values, and other information. River Bend Station utilizes a general license and loads canisters in accordance with the Holtecs HI-STORM 100, Amendment 5, and Final Safety Analysis Report (FSAR), Revision 7. River Bend Station had 23 loaded HI-STORM 100S Version B casks containing MPC-68 canisters at the ISFSI at the time of the routine inspection.

The inspectors requested documentation related to maintenance of the fuel building cask handling crane, the annual maintenance of the licensees special lifting devices, and the annual maintenance of the sites loaded HI-STORM casks and ISFSI pad.

Documents were provided that demonstrated the fuel building cask handling crane was inspected on an annual basis in accordance with the American Society of Mechanical Engineers B30.2 safety requirements. The annual maintenance as required by American National Standards Institute N14.6 for special lifting devices was completed for the following special lifting devices: the HI-TRAC lifting trunnions, lift yoke, lift yoke extension, and the HI-STORM/HI-TRAC lifting brackets. All equipment passed the visual inspection, the dimensional testing, and either the magnetic particle or liquid penetrant non-destructive examinations. The licensee had completed annual inspection and maintenance of their loaded HI-STORM casks and ISFSI pad in accordance with FSAR Table 9.2.1 for two calendar years that were reviewed, 2014 and 2015.

Inspectors reviewed the radiological conditions at the RBS ISFSI through a document review of the most recent radiological survey and three calendar years of thermoluminescent dosimeter monitoring data from around the ISFSI. A dry cask loading supervisor and one radiation protection (RP) technician accompanied the NRC inspectors during a walk-down of the ISFSI pad. A radiological survey was performed by the RP technician to record gamma exposure rates. The measurements taken by the RP technician were consistent with measurements recorded on the most recent ISFSI site survey. The radiological conditions in and around the ISFSI were as expected for the age and heat load of the 23 currently loaded spent fuel storage casks. Annual Radiological Environmental Operating Reports for the RBS site were reviewed for the last two calendar years. The reports documented the dose equivalent to any real individual located beyond the site controlled area had been well below the 10 CFR 72.104(a)(2) requirement of less than 25 millirem per year.

A review of the CAP associated with the ISFSI was conducted by the NRC inspectors. A list of CRs issued since the last NRC ISFSI inspection was provided by the licensee for the cask handling crane and ISFSI operations. When a problem was identified, the licensee would document the issue as a CR in the licensees CAP.

Of the list of CRs provided relating to the ISFSI and the cask handling cranes, 12 were selected by the NRC inspectors for further review. The CRs were related to a variety of issues. The CRs reviewed were well documented and properly categorized based on the safety significance of the issue. The corrective actions taken were appropriate for the situations. Based on the comprehensiveness of the CRs, the licensee demonstrated a high attention to detail in regard to the maintenance and operation of their ISFSI program and the cask handling crane. No NRC safety concerns were identified related to the CRs reviewed.

The licensees 10 CFR 72.48 screenings and evaluations for ISFSI program changes since the last NRC routine ISFSI inspection were reviewed to determine compliance with regulatory requirements. The RBS had not performed any 10 CFR 72.48 full evaluations since the last NRC ISFSI inspection. The NRC inspectors reviewed one 10 CFR 72.48 screen for a modification to the slopes surrounding the ISFSI. River Bend Station had installed concrete canvas sheets over the slopes to provide erosion protection. The one screening reviewed was determined to be adequately evaluated by the licensee. The licensee had made no 10 CFR 50.59 screenings or evaluations associated with the fuel building cask handling crane since the last inspection.

An onsite review of the Quality Assurance audits and surveillance reports related to dry cask storage activities at the RBS ISFSI was performed by the NRC inspectors. The Quality Assurance audit reports and surveillances resulted in several CRs. The NRC inspectors reviewed the corrective actions resulting from the CRs to ensure that the identified deficiencies were properly categorized based on their safety significance and properly resolved. All identified deficiencies had been properly categorized and resolved by the licensee.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On May 12, 2016, the inspectors debriefed Mr. W. Maguire, Site Vice President, and other members of the licensees staff of the results of the routine ISFSI inspection documented in Section 4OA5. Licensee personnel acknowledged the information presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered propriety. No propriety information was identified.

On June 13, 2016, the inspectors presented the radiation safety inspection results to Mr. M. Chase, Director of Regulatory and Performance Improvement, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On July 18, 2016, the inspectors presented the inspection results to Mr. W. Maguire, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

D. Burnett, Director, Emergency Planning, Entergy South
J. Campbell, ISFSI Project Manager
J. Carter, Engineering
M. Chase, Director, Regulatory & Performance Improvement
B. Cole, Senior Manager, Fleet Radiation Protection
R. Conner, Manager, Nuclear Oversight
R. Cook, Manager, Security
K. Crissman, Senior Manager, Maintenance
D. Fletcher, Manager, Supply Chain
B. Ford, Senior Manager, Fleet Regulatory Assurance
T. Gates, Manager, Operations Support
J. Henderson, Manager, Systems & Components Engineering
R. Hite, Supervisor, Radiation Protection
K. Huffstatler, Acting Manager, Regulatory Assurance
R. Leasure, Superintendent, Radiation Protection
P. Lucky, Manager, Performance Improvement
W. Maguire, Site Vice President
C. Miller, Manager, Site Projects and Maintenance Services
P. OConner, Manager, Training
S. Peterkin, Manager, Radiation Protection
J. Reynolds, Senior Manager, Operations
C. Rich, General Manager, Plant Operations
D. Sandlin, Manager, Design & Program Engineering
T. Schenk, Manager, Emergency Preparedness
S. Vazquez, Director, Engineering
T. Venable, Assistant Manager, Operations
J. Vukovics, Supervisor, Reactor Engineering
J. Wieging, Senior Manager, Production
J. Wilson, Manager, Chemistry

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000458/2016002-01 NCV Failure to Follow Station Guidance on Use of Temporary Power Cables and Control of Transient Combustibles (Section 1R05)
05000458/2016002-02 NCV Failure to Conduct Common Cause Failure Evaluation in Response to Inoperable Emergency Diesel Generator (Section 4OA2.2)
05000458/2016002-03 NCV Failure to Identify and Correct Improperly Stowed Transient Combustibles (Section 4OA2.3)

Closed

05000458/2015-009-01 LER Automatic Reactor Scram Due to Partial Loss of Offsite Power Caused by Fault in Local 230kV Switchyard (Section 4OA3.1)

200049/2012001-0 URI Fuel Assemblies Minimum Enrichment is Not Bounded by Offsite Dose Calculation Required by 10 CFR 72.104 (Section 4OA3.2)

LIST OF DOCUMENTS REVIEWED