IR 05000220/2007002
Download: ML071200236
Text
April 27, 2007
Mr. Kevin J. NietmannActing Vice President Nine Mile Point Nine Mile Point Nuclear Station, LLC P.O. Box 63 Lycoming, NY 13093
SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTIONREPORT 05000220/2007002 and 05000410/2007002
Dear Mr. Nietmann:
On March 31, 2007, the US Nuclear Regulatory Commission (NRC) completed an inspection atyour Nine Mile Point Nuclear Power Plant Unit 1 and Unit 2. The enclosed inspection report documents the inspection results discussed on April 20, 2007, with Mr. Mark Schimmel and other members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.This report documents one finding of very low safety significance (Green). The finding wasdetermined to involve a violation of NRC requirements. However, because of its very low safety significance and because it was entered into your corrective action program (CAP), the NRC is treating this violation as a non-cited violation (NCV) in accordance with Section VI.A.1 of the NRC's Enforcement Policy. If you contest the NCV in this report, you should provide a response with the basis for your denial, within 30 days of the date of this inspection report, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C.
20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-001; and the NRC Resident Inspector at Nine Mile Point.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and itsenclosure, and your response (if any) will be available electronically for public inspection in the K. Nietmann2NRC Public Document Room or from the Publicly Available Records (PARS) component of theNRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/Blake D. Welling, Acting ChiefProjects Branch 1 Division of Reactor ProjectsDocket No.:50-220, 50-410License No.: DPR-63, NPF-69
Enclosure:
Inspection Report 05000220/2007002 and 05000410/2007002
w/Attachment:
Supplemental Informationcc w/encl:M. J. Wallace, President, Constellation Generation J.M. Heffley, Senior Vice President and Chief Nuclear Officer C. W. Fleming, Esquire, Senior Counsel, Constellation Energy Group, LLC M. J. Wetterhahn, Esquire, Winston and Strawn P. Smith, President, New York State Energy, Research, and Development Authority J. Spath, Program Director, New York State Energy Research and Development Authority P. D. Eddy, Electric Division, NYS Department of Public Service C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law Supervisor, Town of Scriba T. Judson, Central NY Citizens Awareness Network D. Katz, Citizens Awareness Network
SUMMARY OF FINDINGS
...................................................iii
REPORT DETAILS
..........................................................1
REACTOR SAFETY
.........................................................11R01Adverse Weather Protection .......................................1
1R04 Equipment Alignment ............................................2
1R05 Fire Protection .................................................3
1R08 Inservice Inspection Activities ......................................3
1R11 Licensed Operator Requalification Program ...........................5
1R12 Maintenance Effectiveness ........................................61R13Maintenance Risk Assessments and Emergent Work Control..............71R15Operability Evaluations ...........................................81R19Post Maintenance Testing .........................................91R20Refueling and Other Outage Activities ..............................101R22Surveillance Testing ............................................11
1R23 Temporary Plant Modifications ....................................14
1EP6Drill Evaluation
OTHER ACTIVITIES
........................................................154OA2Identification and Resolution of Problems............................154OA3Event Followup ................................................15 4OA5Other Activities.................................................16 4OA6Meetings, Including Exit..........................................17ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
................................................A-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
...........................A-1
LIST OF DOCUMENTS REVIEWED
..........................................A-1
LIST OF ACRONYMS
.....................................................A-10
iiiSUMMARY
- OF [[]]
FINDINGSIR 05000220/2007002, 05000410/2007002; 01/01/2007-03/31/2007; Nine Mile Point, Units 1and 2; Surveillance Testing.The report covered a thirteen-week period of inspection by resident and region-basedinspectors. One Green NCV was identified. The significance of most findings is indicated by
their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
"Significance Determination Process." Findings for which the significance determination
process does not apply may be Green or be assigned a severity level after NRC management
review. The NRC's program for overseeing the safe operation of commercial nuclear power
reactors is described in
- NUR [[]]
EG-1649, "Reactor Oversight Process," Revision 4, dated
December 2006.
- A.NRC -Identified and Self-Revealing FindingsCornerstone: Mitigating Systems*Green. A self-revealing, non-cited violation (
NCV) of technical specification (TS)5.4, "Procedures," was identified on January 11, 2007, when the Unit 2 reactor
core isolation cooling (RCIC) system automatically isolated as a result of an
improperly performed surveillance procedure. When performing a test of the
temperature instrument that provides residual heat removal (RHR) and
- RC [[]]
system high area temperature isolations, technicians failed to ensure that the
affected channel was bypassed prior to disconnecting the input thermocouple.
This resulted in an automatic isolation of the
- RC [[]]
IC system steam supply and the
unavailability of
- RC [[]]
IC for approximately four hours. Operators immediately
recognized the error and halted the surveillance procedure. Technicians
reconnected the thermocouple, and operators restored
- RC [[]]
IC to a normal
standby lineup.
CAP as condition report (CR)
2007-0186.The finding is greater than minor because it is associated with the humanperformance attribute of the Mitigating Systems cornerstone and affected the
cornerstone objective to ensure the availability, reliability, and capability of
systems that respond to initiating events to prevent undesirable consequences.
The finding is of very low safety significance in accordance with IMC 0609,
Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., "Determining the Significance of Reactor Inspection Findings for
At-Power Situations," based on a Phase 3 analysis. The Region I senior reactor
analyst (SRA) used the Nine Mile Point Unit 2 Standardized Plant Analysis Risk
(SPAR) model and the actual four-hour exposure time to determine that the
increase in core damage frequency was in the range of one core damage
accident in 125,000,000 years of reactor operation, high E-9 per year. This
finding has a cross-cutting aspect in the area of human performance because
the technicians failed to use appropriate human error prevention techniques,
such as self-checking and prominent visual identification of critical procedure
steps. (Section 1R22) B.Licensee-Identified ViolationsNone.
EnclosureREPORT
- DETAIL [[]]
SSummary of Plant StatusNine Mile Point Unit 1 (Unit 1) began the inspection period at 100 percent power. OnJanuary 30, 2007, Unit 1 began coastdown (gradual reduction of reactor power due to fuel
depletion) to refueling outage 19 (RFO19). The plant was shut down on March 17, 2007, to
commence
- RFO 19, which was in-progress at the end of the inspection period.Nine Mile Point Unit 2 (Unit 2) began the inspection period at 100 percent power. OnMarch 8, 2007, the 'A' reactor recirculation pump (
RRP) was secured due to seal degradation.
This caused power to be reduced to approximately 60 percent. A reactor shutdown was
commenced, and the plant reached cold shutdown on March 9, 2007. Following replacement of
the 'A' RRP seal, a reactor startup was commenced on March 14, 2007. Unit 2 achieved
100 percent power on March 18, 2007, and remained there for the rest of the inspection period.1.REACTOR
- SAFETY "Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01Adverse Weather Protection ([[Inspection procedure" contains a listed "[" character as part of the property label and has therefore been classified as invalid. - 2 samples) a.Inspection ScopeThe inspectors completed the following two adverse weather protection samples thisinspection period. *On January 31, 2007, the inspectors reviewed]]
NMPNS's actions regarding thehigh potential for frazil ice intrusion into the Unit 1 intake structure. The
inspectors verified that operators implemented actions and monitoring specified
by the circulating water system operating procedure (OP). The inspectors also
verified that appropriate procedures were in place for loss of intake water level.
Documents reviewed for this inspection are listed in the Attachment.*On February 14, 2007, the inspectors reviewed roof loading design bases forstation structures that are important to safety due to the accumulation of recent
near-record snowfalls. The inspectors verified by discussion with
- NMP [[]]
NS that
measurements of accumulated roof snow were being taken to confirm that actual
loading was within design limits. Documents reviewed included the Updated
Final Safety Analysis Reports (UFSARs) and Individual Plant Evaluations forExternal Events (IPEEE). b.FindingsNo findings of significance were identified.
2Enclosure1R04Equipment Alignment (71111.04 - 4 samples, 71111.04S - 1 sample).1Partial System Walkdown a.Inspection Scope The inspectors performed four partial system walkdowns to verify a train was properlyrestored to service following maintenance or to evaluate the operability of one train while
the opposite train was inoperable or out of service for maintenance and testing. The
inspectors compared system lineups to system OPs, system drawings, and the
applicable chapters in the
- UFS [[]]
AR. The inspectors also verified the operability of critical
system components by observing component material condition during the system
walkdown and reviewing the maintenance history for each component. Documents
reviewed during this inspection are listed in the Attachment. The inspectors performed
partial walkdowns of the following systems:*Unit 2 'B'
RHR subsystem being inoperable forplanned maintenance on January 17, 2007;*Unit 1 primary containment vacuum relief system during planned maintenanceon torus-to-drywell vacuum relief valve 68-02 on January 22, 2007;*Unit 2 Division 1 and 2 125 Vdc electrical systems due to safety significance onMarch 14, 2007; and*Unit 2 Division 3 emergency diesel generator (EDG) following completion ofplanned maintenance on January 27, 2007. b.FindingsNo findings of significance were identified..2Complete System Walkdown a.Inspection Scope The inspectors performed a complete walkdown of accessible portions of the Unit 1 corespray system to identify any discrepancies between the existing equipment lineup and
the specified lineup. During the walkdown, system drawings and OPs were used to
verify proper equipment alignment and operational status. The inspectors reviewed the
open maintenance work orders (WOs) on the system for any deficiencies that could
affect the ability of the system to perform its function. Documentation associated with
unresolved design issues such as temporary modifications, operator workarounds, and
items tracked by plant engineering were also reviewed to assess their collective impact
on system operation. In addition, the inspectors reviewed the CR database to verify that
equipment alignment problems were being identified and appropriately resolved.
Documents reviewed for this inspection are listed in the Attachment.
3Enclosure b.FindingsNo findings of significance were identified.1R05Fire Protection (71111.05Q - 13 samples) a.Inspection ScopeThe inspectors completed 13 quarterly fire protection inspection samples. Theinspectors toured 13 areas important to reactor safety at the station to evaluate
- NMP [[]]
NS's control of transient combustibles and ignition sources and the material
condition, operational status, and operational lineup of fire protection systems includingdetection, suppression and fire barriers. The inspectors used procedure
INV-02,
"Control of Material Storage Areas," the fire hazards analysis and pre-fire plans in
performing the inspection. Documents reviewed are listed in the Attachment. The
areas inspected included: *Unit 1 heater bays;*Unit 1 condenser bay;
- Unit 1 reactor building (RB) southeast corner room;
- Unit 1 RB southwest corner room;
- Unit 2 Division 1 switchgear room;
- Unit 2 Division 2 switchgear room;
- Unit 2 Normal (non-divisional) switchgear rooms
- Unit 2 heater bays;
- Unit 2 steam tunnel;
- Unit 2 south auxiliary bay 215 foot elevation;
- Unit 2 south auxiliary bay 196 foot elevation;
- Unit 2 'A'
RB 175 foot elevation; and
- Unit 2 'C'
- RB 175 foot elevation. b.FindingsNo findings of significance were identified.1R08Inservice Inspection Activities (71111.08 - 9 samples) a.Inspection ScopeThe purpose of this inspection was to assess the effectiveness of
ISI) program for monitoring degradation of the reactor coolant system (RCS)
boundary, risk significant piping system boundaries, and the containment boundary.
The inspectors assessed the ISI activities using the criteria specified in the American
Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code,Section XI
and applicable NRC regulatory requirements. Documents reviewed for this inspection
are listed in the Attachment.
4EnclosureThe inspectors selected a sample of nondestructive examination (NDE) activities forobservation and evaluation for compliance with the requirements of
XI.
The inspectors also selected samples of activities associated with the repair of safety
related pressure boundary components. The sample selection was based on the
inspection procedure objectives, risk significance and availability. Specifically, theinspectors focused on components and systems where degradation would result in a
significant increase in risk of core damage. This sample selection included the review of
nondestructive tests performed on dissimilar metal welds of piping to the reactor
pressure vessel (RPV) nozzles, butt welds of pipe to fitting and pipe to valves in the core
spray system and integral attachment welds to the containment spray system. The
inspectors reviewed the disposition of the results of the ultrasonic test (UT) of the RPV
N2D recirculation nozzle. This test identified an indication that exceeded the
acceptance criteria of
XI. The inspectors reviewed the analytical analysis
(NMP-29Q-301) of the indication that was performed in accordance with the
requirements of
XI, IWB-3600. The analysis concluded that the flaw
indication was acceptable without repair or rework for one additional refueling cycle at
which time (2009) it would be reexamined by UT.The inspectors performed an evaluation of work activities during a drywell entry thisinspection and noted the corrosion and loss of coating on the reactor building closed
loop cooling piping. The condition had been previously noted by
- NMP [[]]
NS but the
inspectors requested an updated evaluation of the condition that was provided in the
disposition of CR 2007-1905. The updated ultrasonic wall thickness measurements
verified that the structural integrity and pressure retention capabilities of the piping was
maintained within specification requirements.The inspectors reviewed portions of the in-process remote visual examination (VT) ofthe steam dryer and observed portions of the replacement of component parts of the
in-vessel shroud tie rod assemblies. The inspectors reviewed a sample of CRs that
were initiated as a result of the inspections performed in accordance with
program. The inspectors reviewed the problem identification, cause analysis and
corrective actions provided in the disposition of the selected CRs. The inspectors
evaluated these activities for compliance with the requirements of the
- AS [[]]
XVI.The inspectors performed a direct observation of three nondestructive tests and alsoperformed a documentation review of two tests that included both volumetric and
surface examinations. The inspectors also performed a VT of selected areas of the
containment liner to assess the condition of the liner coating. As a result of the
inspectors' examination, supplemental inspection was performed to acquire additional
liner wall thickness measurements. WO 07-03718-00 was initiated to provide
instructions for surface preparation to accommodate thickness testing. Thickness
measurements were specified in action item four of the disposition to CR 2007-1695 and
recorded in
NDEs were reviewed:*UT, volumetric examination, weld # 40-WD-045, butt weld, pipe to elbow, corespray system (40);
5Enclosure*UT, volumetric examination, weld # 40-WD-047, butt weld, pipe to valve, corespray system (40);*Magnetic particle test (MT), surface examination, containment spray,W-1-4.00-07-012, pipe to saddle weld #80-13-WD-001;*Liquid penetrant test (PT), surface examination, weld 33.2-6-R05-WD-001,integral attachments to reactor water clean up (RWCU) piping, data report
W-1-3.00-07-001; and*VT-1, visual surface examination of damage of the
- NDE report 1-2.01-07-0042.The inspectors selected a sample of repair/rework activities for review that required thedevelopment and implementation of an
XI repair plan. The inspectors
reviewed documentation for the planned weld repair on the pressure boundary of two
WO 05-12874-02 was initiated for the weld repair of the
heat exchanger stationary channel cover on Unit
EGS*E1C that
involved restoration of corroded locations and sealing surfaces by depositing weld metal
on an
WO 07-03643-00 was
initiated for the rework of damage to the reactor head and vessel flange in the vicinity of
stud #27. The inspectors reviewed the
XI plans, work scope, activity
sequence, weld filler metal selection, weld procedure specifications and procedure
qualification records (PQR), welder qualifications, specified non-destructive tests,
acceptance criteria and post work testing.The inspectors selected two CRs for review in which a nondestructive examinationidentified a nonconforming condition that was accepted for continued service without
repair or rework. Components identified in
2007-1477 (reactor building closed loop cooling pipe support) were visually inspected
and nonconforming conditions were noted that were evaluated and accepted for
continued service without repair or rework. b.FindingsNo findings of significance were identified.1R11Licensed Operator Requalification Program (71111.11Q - 2 samples) a.Inspection ScopeThe inspectors completed two licensed operator requalification training program (LORT)inspection samples. Documents reviewed for this inspection are listed in the
Attachment. For each scenario observed the inspectors assessed the clarity and
effectiveness of communications, the implementation of appropriate actions in response
to alarms, the performance of timely control board operation and manipulation, and the
oversight and direction provided by the shift manager. During the scenario the
inspectors also compared simulator performance with actual plant performance in the
control room. The following simulator scenarios were observed:
6Enclosure*On February 9, 2007, the inspectors observed Unit
- 1 LO [[]]
RT to assess operatorand instructor performance during a scenario involving a feedwater pump trip,
turbine vibrations, and a steam leak in containment that required initiation of
containment spray. The inspectors evaluated the performance of risk significant
operator actions including the use of emergency operating procedures (EOPs,)
N1-EOP-2, "RPV Control," and N1-EOP-4, "Primary Containment Control."*On March 2, 2007, the inspectors observed Unit
- 2 LO [[]]
RT to assess operator andinstructor performance during a scenario that involved a steam leak in the
drywell followed by a reactor scram in which several control rods failed to insert.
The inspectors evaluated the performance of risk significant operator actions
including the use of
EOP-C5, "Failure to Scram," and N2-EOP-PC,
"Primary Containment Control." b.FindingsNo findings of significance were identified.1R12Maintenance Effectiveness (71111.12Q - 2 samples) a.Inspection ScopeThe inspectors completed two maintenance effectiveness inspection samples. Theinspectors reviewed performance-based problems involving selected in-scope
structures, systems, or components (SSCs) to assess the effectiveness of the
maintenance program. Reviews focused on: proper Maintenance Rule (MR) scoping in
accordance with 10 CFR 50.65; characterization of reliability issues; changing system
and component unavailability; 10 CFR 50.65 (a)(1) and (a)(2) classifications; identifying
and addressing common cause failures, trending key parameters, and the
appropriateness of performance criteria for SSCs classified (a)(2) as well as the
adequacy of goals and corrective actions for SSCs classified (a)(1). The inspectors
reviewed system health reports, maintenance backlogs, and MR basis documents.
Other documents reviewed for the inspection are listed in the Attachment. The following
two
EC) system performance; and*Unit 2 EDG ventilation system motor operated damper failures. b.FindingsNo findings of significance were identified.
7Enclosure1R13Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples) a.Inspection Scope The inspectors reviewed risk assessments for the following eight work weeks during theinspection period. The inspectors verified that risk assessments were performed in
accordance with
OPS-117, "Integrated Risk Management," that risk of scheduled
work was managed through the use of compensatory actions and schedule adherence;
and that applicable contingency plans were properly identified in the integrated work
schedule. Documents reviewed for the inspection are listed in the Attachment. The following workweeks were reviewed:Unit 1*Week of January 22, 2007, that included a two-day rebuild of the actuator fortorus-to-drywell vacuum relief valve 68-02, a containment spray loop 112
quarterly surveillance, and a two-day period for annual maintenance on the
diesel fire pump.*Week of January 29, 2007, that included emergent troubleshooting on the maingenerator amplidyne brushes, 115 kilovolt (kV) switchyard relay testing, below
freezing outside air and lake temperatures, and standby liquid control system
and emergency service water system surveillance testing.*Week of February 26, 2007, that included testing and emergent troubleshootingon the
EDG 103 surveillance
testing, planned maintenance on Line 8 345 kV switchyard breakers, and core
spray 111 and 121 surveillance testing.*Week of March 5, 2007, that included planned maintenance on Line 8 345 kVswitchyard breakers, a standby liquid poison system monthly surveillance, and
- EDG raw water system performance testing to evaluate flow degradation.Unit 2*Week of January 15, 2007, that included planned maintenance and testing on 'A'
RHR system, 345 kV switchyard protective relay testing, and low pressure core
spray and Division
- 1 EDG testing. *Week of January 22, 2007, that included planned maintenance on the highpressure core spray system, the Division 3
EDG, and the 'F' service water pump
and strainer. *Week of February 12, 2007, that included planned maintenance and testing onthe Division
RHR system testing.*Week of March 5, 2007, that included a Division 2 EDG monthly surveillance,Division 2 loss of offsite power / loss of coolant accident quarterly relay testing,
and a standby liquid control system quarterly surveillance. b.Findings
8EnclosureNo findings of significance were identified.1R15Operability Evaluations (71111.15 - 8 samples) a.Inspection Scope The inspectors reviewed operability determinations associated with the eight CRs listedbelow. The inspectors evaluated the acceptability of the selected determinations; when
needed, the use and control of compensatory measures; and the compliance with TSs.
The inspectors' review verified that the operability determinations were made as
specified by procedure
NL-1.01-1003, "Conduct of Operability Determinations."
The technical adequacy of the determinations was reviewed and compared to the
- UFS [[]]
AR, Technical Requirements Manual and associated design basis documents
(DBD.) Other documents reviewed for this inspection are listed in the Attachment. The
following eight evaluations were reviewed:*CR-2006-5855 concerning the hinge pin cover leak on feedwater supply checkvalve
- CR -2007-0300 concerning the automatic scram that occurred at MonticelloNuclear Station after all four turbine control valves opened unexpectedly;*CR-2007-0448 concerning the spiking on local power range monitor,
- APRM 14;*CR 2007-0181 and 2007-0211 concerning an intermittent closed positionindicating light for Unit 1 electromatic relief valve,
CR 2007-0870 concerning a 10 CFR 50 Part 21 notification on non-conservativeassumptions in the design analysis of the Unit 2 emergency core cooling system
strainer crush pressure;*CR 2007-0838 concerning
EC system insulation in preparation for the refueling outage;*CR 2007-0869 concerning requirements for maintaining the automatic isolationfunction of the shutdown cooling system isolation valves during cold shutdown
and refueling; and*CR 2007-1090, concerning continued operation with packing leakage from theRCIC system steam supply outboard containment isolation valve,
MOV121. b.FindingsNo findings of significance were identified.
9Enclosure1R19Post Maintenance Testing (71111.19 - 8 samples) a.Inspection ScopeThe inspectors completed eight post maintenance testing inspection samples. Theinspectors reviewed post maintenance test procedures and associated testing activities
for selected risk significant Mitigating Systems to assess whether the effect of
maintenance on plant systems was adequately addressed by control room and
engineering personnel. The inspectors verified that test acceptance criteria were clear;
demonstrated operational readiness and were consistent with DBDs; that test
instrumentation had current calibrations and the range and accuracy for the application;
and that tests were performed, as written, with applicable prerequisites satisfied. Upon
completion, the inspectors verified that equipment was returned to the proper alignment
necessary to perform its safety function. The adequacy of the identified post
maintenance testing requirements were verified through comparisons with the
recommendations of
SAT-02, "Pre/Post-Maintenance Test Requirements," and the
design basis documentation contained in the
UFSAR and associated design basis
documentation. Other documents reviewed for this inspection are listed in the
attachment. The following post-maintenance test activities were reviewed:*Unit 1,
BV68-02. The retest was performed in accordance with N1-ST-SA6, "Drywell/Torus and
Torus/RB Vacuum Reliefs Test," and N1-ST-R11, "Valve Remote Position
Indicator Verification." *Unit 1,
WO-06-20636-00 that performed annualpreventative maintenance and engine speed adjustments for the diesel fire
pump. The retest was performed in accordance with N1-PM-W9, "Fire
Protection System - Weekly Operation of Fire Pumps." *Unit 2,
RPV isolation check valve 2FWS*23B. The retest was performed in
accordance with N2-ISP-LRT-R@102, "Type "C" Containment Isolation Valve
Vacuum Leak Rate Test
LV-10B. The retest was performed in
accordance with the
EPM-GEN-063, "Limitorque
- WO 07-01313-00 that replaced reactor protection system relayC72A-K14L. The retest was performed in accordance with N2-
"Channel Scram Response Time Test," and N2-OSP-RPS-W002, "Manual
Scram Channel Functional Test."*Unit 2,
- WO s 05-02332-00 and 05-01272-00 that performed maintenance onservice water pump 'F' discharge strainer, 2
SWP*STR4F, and discharge check
valve, 2SWP*V1F. The retest was performed in accordance with
N2-OSP-SWP-Q002, "Service Water Pump and Valve Operability Test," and
N2-OSP-SWP-Q004, "Division 2 Service Water Operability Test."
10Enclosure*Unit 2,
MOV4C. The retest was performed in accordance
with N2-OSP-RHS-Q003, "RHR System Loop C Valve Operability Test." *Unit 2,
EDG and auxiliary equipment. The retest was performed in
accordance with N2-OSP-EGS-M@002, "Diesel Generator and Diesel Air Start
Valve Operability Test - Division III." b.FindingsNo findings of significance were identified.1R20Refueling and Other Outage Activities (71111.20 - 1 sample) a.Inspection Scope Forced Outage 2F701: The inspectors observed and reviewed the following activitiesduring the Unit 2 forced outage F701 from March 8 to March 16, 2007. Documents
reviewed for this inspection are listed in the Attachment.*The inspectors observed portions of the plant shutdown and cooldown andverified that the
- TS cooldown rate limits were satisfied.*The inspectors reviewed outage schedules and procedures and verified that
TSrequired safety system availability was maintained, shutdown risk was
considered, and that contingency plans existed to restore key safety functions
such as electrical power and containment integrity.*The inspectors performed a walkdown of the drywell to identify evidence of RCSleakage, and verify the condition of drywell coatings, structures, valves, piping,
supports and other equipment. The inspectors also verified that no debris was
left in the drywell that could affect the performance of the emergency core
cooling system suction strainers.*The inspectors observed portions of the reactor startup following the outage, andverified through plant walkdowns, control room observations, and surveillance
tests (ST) reviews that safety-related equipment required for mode change was
operable.Refueling Outage 1RFO19: The inspectors observed and/or reviewed the following Unit1 refueling outage activities to verify that operability requirements were met and that
risk, industry experience, and previous site specific problems were considered. The
refueling outage and inspection sample were in-progress at the end of the inspection
period. Documents reviewed for this inspection are listed in the Attachment.*The inspectors reviewed outage schedules and procedures, and verified thatTS-required safety system availability was maintained and shutdown risk was
minimized. The inspectors verified that when specified by
- NUMA [[]]
RC 91-06,
"Guidelines for Industry Actions to Assess Shutdown Management," and
- NMP [[]]
- OUT -01, "Shutdown Safety," contingency plans existed forrestoring key safety functions. *The inspectors observed portions of the plant shutdown and cooldown onMarch 17 and verified that the
NMPNS maintained andadequately protected electrical power supplies to safety-related equipment and
that TS requirements were met.*The inspectors verified proper alignment and operation of shutdown cooling andother decay heat removal systems. The verification also included reactor cavity
and fuel pool makeup paths and water sources and administrative control of
drain down paths.*The inspectors reviewed N1-FHP-25, "General Description of Fuel Moves,"N1-FHP-27C, "Core Shuffle," N1-ODP-NFM-101, "Refueling Operations," and
TS, and verified all requirements for refueling operations were met through refuel
bridge observations, control room panel walkdowns and surveillance procedure
reviews.*After the drywell was opened for general access, the inspectors performed an"as-found" walkdown to identify evidence of RCS leakage and verify the
condition of drywell structures, piping, and supports. b.FindingsNo findings of significance were identified.1R22Surveillance Testing (71111.22 - 8 samples) a.Inspection ScopeThe inspectors completed eight quarterly surveillance testing inspection samples. Theinspectors witnessed performance of and/or reviewed test data for eight risk-significant
UFSAR, Technical Requirements
Manual, and
- NMP [[]]
NS procedure requirements. The inspectors verified that test
acceptance criteria were clear, demonstrated operational readiness and were consistent
with the DBDs; that test instrumentation had current calibrations and the range and
accuracy for the application; and that tests were performed, as written, with applicable
prerequisites satisfied. Upon ST completion, the inspectors verified that equipment was
returned to the status specified to perform its safety function. Documents reviewed for
this inspection are listed in the Attachment. The following eight
TE49D;"*N1-ST-Q6C, "Containment Spray System Loop 112 Quarterly Operability Test;"
- N2-OSP-RHS-Q@006, "RHR System Loop C Pump and Valve Operability Testand System Integrated Test;"*N1-ST-Q1B, "Core Spray 121 Pump, Valve and Shutdown Cooling Water SealCheck Valve Operability Test;"
2Enclosure*N1-ST-R9, "Core Spray Operability Test Using Demineralized Water;" *N1-ST-M4A, "EDG 102 and PB 102 Operability Test;"
- N2-OSP-CSH-Q@002, "High Pressure Core Spray Pump and Valve Operabilityand System Integrity Test;" and*N2-OSP-EGS-M@002, "Diesel Generator and Diesel Air Start Valve OperabilityTest - Division
RCIC system automatically isolated as a result of an
improperly performed surveillance procedure. When performing a test of the
temperature instrument that provides
RCIC system high area temperature
isolations, technicians failed to ensure that the affected channel was bypassed prior to
disconnecting the input thermocouple. This resulted in an automatic isolation of the
- RCIC system steam supply.Description. On January 11, 2007, instrument and controls technicians were performinga quarterly
systems. This function was provided by four channels of the reactor building (RB)
ambient temperature instrumentation. The test was performed using a test device in
place of the instrument channel input thermocouple to verify the high temperature
isolation setpoint. To prevent inadvertent actuation prior to disconnecting the input
thermocouple to install the test device, the associated system automatic isolation
function must be bypassed. This was done using a keylocked
RCIC isolation
bypass switch.The surveillance procedure, N2-ISP-LDS-Q007, "Quarterly Functional Test of
TE49D," contained separateand similar attachments for each of the four temperature instrument channels. After
successfully completing the first two attachments, the technicians went on to test the
third temperature channel. However, in this case, the lead technician signed the
procedure to indicate that the
RCIC isolation switch had been placed in "bypass"
before it was actually completed. The lead technician then directed the technician to
disconnect the thermocouple. Because the
RCIC isolation switch was not in the
"bypass" position, this caused an automatic isolation of the
- RC [[]]
IC steam supply.
Operators immediately recognized the error and halted the surveillance procedure.
Technicians reconnected the thermocouple, and operators restored
- RC [[]]
IC to a normal
standby lineup. During the four hours that the
- RC [[]]
- RCIC system is 14 days.Analysis. The performance deficiency associated with this event was that techniciansdid not properly follow a surveillance test procedure, which caused the Unit 2
system to automatically isolate, rendering the system unavailable to perform its safety
function. The procedure directed operators to place the
RCIC isolation bypass
13Enclosureswitch in the "bypass" position and to verify that the switch was in "bypass" by twoindependent means prior to disconnecting the thermocouple. The technician did not
perform these steps but marked them completed. The finding is greater than minor
because it was associated with the human performance attribute of the Mitigating
Systems cornerstone and adversely affected the cornerstone objective to ensure the
availability, reliability, and capability of systems that respond to Initiating Events to
prevent undesirable consequences. The finding was determined to be of very low
safety significance in accordance with IMC 0609, Appendix A, "Determining the
Significance of Reactor Inspection Findings for At-Power Situations." The inspectors
evaluated the significance of this finding using IMC 0609, Appendix A, Phase 1, and
determined that a Phase 2 analysis was required because the finding represented an
actual loss of the
determined that a Phase 3 analysis was necessary because the site-specific Phase 2
notebook indicated that the finding could be more than of very low safety significance
assuming an exposure time of three days. The
- SP [[]]
AR model and the actual four-hour exposure time to determine that the increase in
core damage frequency was in the range of 1 core damage accident in 125,000,000
years of reactor operation, high E-9 per year. The
- SP [[]]
AR model dominant cutsets were
a station blackout with failure of high pressure injection sources and the inability to
restore
SRA concluded that the
finding was of very low safety significance. This finding has a cross-cutting aspect in
the area of human performance because the technicians failed to use appropriate
human error prevention techniques, such as self-checking and prominent visual
identification of critical procedure steps.Enforcement. TS 5.4, "Procedures," states, in part, that, written procedures shall beestablished, implemented, and maintained covering the applicable procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, Item 8, "Procedures for
Control of Measuring and Test Equipment and for STs, Procedures, and Calibrations,"
lists containment isolation tests as an applicable group of tests. Contrary to the above,
Unit 2 Instrument Surveillance Procedure N2-ISP-LDS-Q007, "Quarterly Functional Test
of
TE49D," was not correctlyimplemented. On January 11, 2007, Procedure Attachment 3 step 7.2.1, place and
verify the
RCIC isolation channel bypass switch in the "bypass" position, was not
completed prior to performing Attachment 3 step 7.2.2, to disconnect the associated
channel thermocouple leads. Procedure step 5.2 in Section 5.0 "Limitations and
Actions," states, "Steps in Section 7.0 and 8.0 shall be performed in sequence."
Because this procedural noncompliance is of very low safety significance and was
entered into the
- RC [[]]
IC Steam Supply.1R23Temporary Plant Modifications (71111.23 - 2 samples)
14Enclosure a.Inspection ScopeThe inspectors completed two temporary modification inspection samples. For thetemporary change packages (TCPs) listed below the inspectors verified that the
installation and/or removal of temporary modifications did not affect the safety functions
for the associated systems. The inspectors assessed the adequacy of the 10 CFR 50.59
evaluations; verified that the changes did not adversely affect the system's ability to
perform its design functions as described in the
TS; that the installation and
removal was consistent with the modification documentation; that the drawings and
procedures were updated as applicable; and that the post-installation and restoration
testing was adequate.*TCP No. N2-06-091, Leak Seal for
- 2FWS *23B, Revision 2 b.FindingsNo findings of significance were identified. Cornerstone: Emergency Preparedness1
EP6Drill Evaluation (71114.06 - 1 sample) a.Inspection Scope The inspectors completed one drill evaluation inspection sample. The inspectorsobserved simulator, technical support center and emergency operations facility activities
associated with the Unit 1 emergency planning drill on March 1, 2007. The inspectors
verified that emergency classification declarations and notifications were completed in
accordance with
CFR 50, Appendix E, and the Nine Mile Point
emergency plan implementing procedures. Documents reviewed for this inspection are
listed in the Attachment. b.FindingsNo findings of significance were identified.
15Enclosure4.OTHER
- ACTIVI [[]]
TIES4OA2Identification and Resolution of Problems.1Review of Items Entered into the CAP a.Inspection ScopeAs specified by Inspection Procedure 71152, "Identification and Resolution ofProblems," and in order to help identify repetitive equipment failures or specific human
performance issues for follow-up, the inspectors performed a daily screening of all items
entered into
CAP. The review was accomplished by accessing the
computerized database for
CR screening meetings. In accordance
with the baseline inspection modules the inspectors also selected 73 CAP items across
the Initiating Events, Mitigating Systems, Barrier Integrity, and Public Radiation Safety
cornerstones for additional follow-up and review. The inspectors assessed
- NMP [[]]
NS's
threshold for problem identification, the adequacy of the cause analyses, extent of
condition review, operability determinations, and the timeliness of the specified
corrective actions. The
- OA 3Event Followup (71153 - 2 samples).1Loss of Unit 1 Plant Vent Effluent Normal Monitoring CapabilityOn January 26, the Unit 1 off-gas effluent stack monitoring system (OGESMS) wasdeclared inoperable due to low sample flow. With
- OGES [[]]
MS inoperable, the Offsite
Dose Calculation Manual (ODCM) required that auxiliary sampling be placed in service
within eight hours. However, due to the low sample flow, attempts to place the auxiliary
stack gas sampling system in service were unsuccessful. As a result, Unit 1 could not
satisfy the
- OD [[]]
CM stack sampling requirements for noble gas, particulate, and iodine.
The
- OD [[]]
CM did not specify actions if both the normal and auxiliary sampling systems
were unavailable. Therefore, in response to the event,
- NMP [[]]
NS developed an alternate
monitoring procedure to use in-plant monitoring equipment to estimate stack effluent
release rates.This event occurred during a period of severe winter weather.
- NMP [[]]
NS suspected thecause to be an ice blockage in the common sample line. Because the sample point is
near the top of the plant stack, the weather conditions did not support direct
investigation.
- NMP [[]]
NS attempted to clear the obstruction using heated pressurized
nitrogen. On January 27, 2007, this method was successful, and
- OGES [[]]
MS was
returned to service. However, the sample line again became obstructed on
February 3, 2007, forcing Unit 1 to revert to the alternate monitoring procedure for stack
effluent monitoring. On February 20, 2007, weather conditions moderated to the point
16Enclosurethat the pressurized nitrogen method successfully cleared the sample line and workersreplaced the heat trace and line insulation on the exposed portion of sample line at the
top of the stack.The inspectors reviewed
OGESMS and reviewed thealternate monitoring procedure. The inspectors examined the event in terms of its effect
on
- NMP [[]]
NS's ability to implement their emergency plan, as well as its effects on public
radiation safety. b.FindingsNo findings of significance were identified. .2'A' Reactor Recirculation Pump Seal Degradation (Event Notification 43223)During restoration from a planned power reduction on February 3, 2007, short durationperturbations were observed in normally stable pressures and temperatures associated
with the 'A'
- NMP [[]]
NS suspected that the perturbations were caused by foreign material flushed
through the seal. Operations issued a special order to establish additional monitoring of
seal parameters while changing plant conditions.Infrequent short duration seal parameter perturbations occurred randomly over the nextseveral weeks. On March 8, 2007, a sudden, substantial increase in upper seal cavity
pressure occurred, indicating that the inboard seal had failed. Operators secured and
isolated the 'A'
OP for RRP seal failure. This caused a
power reduction to approximately 60 percent. After stabilizing and assessing plant
conditions, operators proceeded to shut down the plant to repair the 'A'
- NMPNS 's response to the short term seal parameterperturbations, and observed the operators' response to the 'A'
- SBO Coping Time a.Inspection ScopeThis unresolved item was opened to complete a review of the impact of an incorrectprobabilistic risk assessment (
PRA) assumption that there was a high probability that
certain 11 station battery loads would be de-energized (shed) within 15 minutes of the
start of a station blackout (SBO) event. The inspectors considered this assumption
incorrect because the SBO procedure did not direct load shedding until 30 minutes into
17Enclosurethe event, the SBO procedure required other time consuming steps before loadshedding, and the operators would not have secured the loads prematurely because
some loads provided useful indications and alarms. The inspectors reviewed
SAS-04-06, "PRA Margin Assessment for Unit1 Station Blackout DC Load Shedding." Specifically, the inspectors verified that load
shedding times coincided with SBO procedure requirements; that average, realistic
values were used for input assumptions; and that the probability of failing to load shed
was dependent on the failure to meet the procedural load-shedding times.Based on the review of
PRAengineers, the inspectors determined that although the stated time in the PRA for load
shedding during an SBO was incorrect, satisfactory margin remained for 11 station
battery capacity if SBO procedure load shed time requirements were met. No violations
of NRC requirements were identified. This item is closed. b.FindingsNo findings of significance were identified..2Review of the Institute of Nuclear Power Operations 2006 Evaluation a.Inspection ScopeThe inspectors reviewed the interim report of the Institute Nuclear Power OperationsNovember 2006 evaluation of Nine Mile Point dated January 2, 2007. The inspectors
reviewed the report to ensure that issues identified were consistent with the
- NMP [[]]
NS's performance and to identify significant safety issues that
required
- OA 6Meetings, Including ExitExit Meeting SummaryThe inspectors presented the inspection results to Mr. Mark Schimmel and othermembers of
NMPNS acknowledged that
some of the material reviewed by the inspectors during this period was proprietary, but
that the content of this report includes no proprietary information.ATTACHMENT:
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- INFORM [[]]
- POINTS [[]]
- OF [[]]
- CONTAC [[]]
TLicensee personnelN. Conicella, Manager, OperationsR. Dean, Director, Quality and Performance Assessment
M. Faivus, General Supervisor, Chemistry
J. Gerber, General Supervisor, Radiation Protection
J. Laughlin, Manager, Engineering Services
T. Maund, Manager, Maintenance
M. Miller, Director, Licensing
K. Nietmann, Site Vice President
W. Paulhardt, Manager, Integrated Work Management
- LIST [[]]
- OF [[]]
- ITEMS [[]]
- AND [[]]
- DISCUS SEDOpened and Closed05000410/2007002-01NCVFailure to Follow Procedure CausedInadvertent Isolation of
- RC [[]]
IC Steam Supply
(Section 1R22)Closed05000220/2006008-03URIPRA Assumptions Regarding
- OF [[]]
- REVIEW [[]]
CR 2004-0385, Sudden Unit 1 intake structure icing while on reverse flow
N1-OP-19, "Circulating Water System"
N1-SOP-19, "Intake Structure Icing"
N1-SOP-18.1, "Service Water Failure, Low Intake Level"
O1-OPS-001-275-1-01, "Circulating Water System"
O3-OPS-009-JIT-3-01, "Just-in-time training for Plant Startup"
O3-OPS-009-JIT-3-02, "Just-in-time training for Plant Shutdown"
A-2AttachmentCR 2006-4584, Known deficiencies not corrected on equipment important for summerreadiness at Unit 2
Steven F. Daly, Cold Regions Technical Digest No. 91-1, "Frazil Ice Blockages of Intake Trash
Racks," March 1991
TQS-20, "Operator Continuing Training Biennial and Cyclic Schedule Development andMaintenance"
N1-275000-RBO-13, "Events and Human Performance"Section 1R04: Equipment AlignmentUnit
N1-OP-2, "Core Spray System"
N2-OP-31, "RHR System"
N2-VLU-01, "Walkdown Order Valve Lineup and Valve Operations," Attachment 31, "N2-OP-31
Walkdown Valve Lineup"
N2-OP-74A, "Emergency DC Distribution"
N2-OP-71D, "Uninterruptible Power Supplies (UPS)"
PI&R C-18006-C
PI&R C-18007-C
N2-OP-100B, "HPCS Diesel Generator"Section 1R05: Fire ProtectionNine Mile Point Unit
- 2 UFS [[]]
INV-02, Revision 17, Control of Material Storage Areas
N1-FPI-PFP-0101, "Pre-fire Plans," Revision 1
N2-FPI-PFP-0201, "Pre-fire Plans," Revision 0Section 1R08: Inservice Inspection ActivitiesExamination ProceduresNDEP-UT-6.28 R00Ultrasonic Examination of Dissimilar Metal Piping Welds (Manual)PDI-UT-10 Revision A,
UT examination of dissimilar metal piping
- ASME [[]]
XIExamination ReportsW-1-2.01-07-001VT-3 Examination Data of support 70-R19-B, broken bolt headW-1-4.00-07-001Magnetic Particle Examination Data, integral attachments, pipe support,system 93, Containment SprayW-1-3.00-07-001Liquid Penetrant Examination Data, integral attachments, system 33,RWCUW-1.2.01-07-0042VT-1 Examination Report, RPV head flange, slight corrosion deterioration
A-3AttachmentW-1-4.00-07-012Magnetic Particle Examination Data, pipe to saddle weld # 80-13WD001,Reactor Containment SprayW-1-6.24-07-105UT report, Weld # 40-WD-045, butt weld, core spray system
W-1-6.24-07-107UT report, Weld # 40-WD-047, butt weld, pipe to valve, core spraysystemNDE 1-6.05-07-0009UT report, drywell liner thickness data in the vicinity of area coolers #11,15(two locations) and 16. Work Orders07-03643-00RPV flange, repair damage at stud location #27 (vessel flange)
06-18382-00Removal and Installation of Recirculating Pump Seals, 2RCS P1A
05-12874-02Repair of Corroded areas of Channel Cover (2EGS E1C 000)
07-03718-00Ultrasonic Examination Report of wall thickness readings of corrosion onthe drywell linerWelding ProceduresS-MAP-SPC-0102 Welding/Brazing Procedure Specifications (Revision 27)WPS-8-8-BA-102Manual gas tungsten arc welding (GTAW) and shielded metal arc(SMAW) welding of P8 to P8WPS-1-1-BA-101Manual
- SMAW [[]]
- PQR [[]]
- PQR [[]]
- SMAW [[]]
- SMAW [[]]
INSTALL-001 at 90/270 and 350 degreepositionsCN 006503Change Notice - evaluation of core flow/core power effects
- DCP N1-06-090 R00Design Change Procedure - Modify Core Shroud Tie Rod UpperSupport AssembliesAppendix
RBCLC system components
DrawingsE231-563-0Vessel Forming and Welding - Upper
E231-577-0RPV Miscellaneous Details - Head to Vessel O-Rings
E231-575-3RPV Closure Head Final Machining
F-45183-C R4RWCU, weld 33.2-6-R-05-WD-001
R19-B R2RB Closed Loop Cooling, Support 70-R19-B
CalculationsS13.4-70-M003System 70,
- RBC [[]]
LC, Minimum Wall Thickness (1986)
S13.4-70-TP15System 70,
- RBC [[]]
LC, Minimum Wall Thickness (1995)
A-4AttachmentSection 1R11: Licensed Operator RequalificationNMPNS Operations ManualNEI 99-02, "Regulatory Assessment Performance Indicator Guidelines," Revision 4
HU-1.01-1001, "Human Performance Tools and Verification Practices"
S-ODP-OPS-0001, "Conduct of Operations"
N1-SOP-1, "Reactor Scram"
N2-SOP-101C, "Reactor Scram"
N1-EOP-02, "RPV Control"
N1-EOP-05, "Secondary Containment Control"
N2-ARP-01, "Control Room Alarm Response Procedures."
N2-EOP-RPV, "RPV Control"
Unit 1 Alarm response procedures
N1-SOP-31.1, "Turbine Trip"
N1-SOP-16.1, "Feedwater System Failures"
N1-SOP-1.1, "Emergency Power Reduction"
EPP-0101, "Unit 1 Emergency Classification Technical Bases"
N2-SOP-101D, "Rapid Power Reduction"
N2-SOP-08, "Unplanned Power Changes"
N1-EOP-C5, "Failure to Scram"
OPS-009-1DY-2-63, "Feedwater Heater Tube Bundle Leak with
Control Rod Drift/Steam Line Break/ATWS"
OPS-009-1DY-1-57, "Feedwater Pump Trip, Turbine Vibrations,
Steam Leak in Containment"
N2-EOP-PC, "Primary Containment Control"
N1-EOP-4, "Primary Containment Control"
Section 1R12: Maintenance Rule ImplementationNine Mile Point
MR Integrated Scoping Matrix
Unit 1 MR Integrated Performance Criteria Matrix
Unit 1 MR Integrated Performance Criteria Matrix - Super Systems
Unit 1 MR High Safety Significant Functions and Related Key Safety Functions
Unit 1 MR Function Report - Emergency Cooling
Unit 2 MR Integrated Scoping Matrix
Unit 2 MR Integrated Performance Criteria Matrix
Unit 2 MR Integrated Performance Criteria Matrix - Super Systems
Unit 2 MR High Safety Significant Functions and Related Key Safety Functions
Unit
HVP - Diesel Generator Ventilation System
A-5AttachmentNMP -
- MR Category (a)(1) Detailed progress report for Unit 2 diesel generator ventilationsystem motor operated damper failures
HVP*MOD1B failed to
close as designed
MR Category (a)(1) Summary Report for Unit 2 diesel generator ventilation system
motor operated damper failures
- III [[]]
- HVP dampersSection 1R13: Maintenance Risk Assessments and Emergent Work EvaluationGAP-OPS-117, "Integrated Risk Management"GAP-PSH-03, "Control of On-line Work Activities"
- HP [[]]
CS Diesel Generator and auxiliary
equipment
ENG-100-01, engine speed needs to be increased
N1-ST-M4A, "Emergency Diesel Generator 102 and PB 102 Operability Test"
N1-ST-Q16A,"Emergency Diesel Generator 102 Quarterly Test
BV-68-02, disassemble and rebuild actuator, replace o-rings, gaskets, seal
WO 07-01341-00, Re-brush and re-clean main generator amplidyne
N2-ISP-ISC-Q017, "Quarterly Functional Test of Feedwater/Main Turbine Trip on Reactor
Vessel Water High Level 8 Instrument Channels"
N2-OSP-EGS-M@001, "Diesel Generator and Diesel Air Start Valve Operability Test - Division I
and
ICS*PDT168 susceptible to excess instrument drift
and requires replacement
RCIC steam line flow high instrument
channel
N2-ISP-ICS-R121, "Operating Cycle Channel Calibration Including Isolation Time Delay"
SOV maintenance, and
replace pre-filter cartridge
N2-OSP-RHS-M001, "RHR Discharge Piping Fill (LPCI) and Valve Lineup Verification"
A-6AttachmentN2-ISP-RHS-Q022, "Quarterly Functional Test of the
CEC*PNL629 defeat high drywell pressure interlock
N2-ISP-ISC-Q003, Quarterly Functional Test of the Reactor Vessel Water Level Low Low Level
and the Reactor Vessel Low Low Low Water Level 1 Instrument Channels"
N2-OSP-CSL-M001, "LPCS Discharge Fill And Valve Line-up Verification"
N1-ST-Q1A, "CS 111 Pump and Valve And
ESR 05-02712 and ESR 05-3333, this work is to be
performed pre-outage
ST-M4A, "Emergency Diesel Generator 102 and PB 102 Operability
Test"
ST-M4A surveillance when the control switch was taken to stop, not
minute cooldown
ST-M4A when EDG 102 control switch taken
to shutdown position no 3 minute cooldown
N1-ST-Q28, "Containment Spray Raw Water Inter Tie Check Valve Quarterly Operability Test"
Nine Mile Point Site T-0 System Schedules, Schedule Risk Assessment Summary Tables, and
- PRA Work Week Summaries for work weeks 702-705 and 710Section 1R15: Operability EvaluationsEmail dated 01/16/2007, D. Pelton to L. Cline regarding recent event at Monticello
- AS [[]]
ME Code Class 1 and 2
Components"
ACR 06-06587, Hinge Pin cover leaking approximately 100 drops per minute
Design Change Package (DCP) No. N2-01-203, Check Valve Internals Modification
AOV23A/B
Dwg No. 0005360170408, 24 inch, 900 lb., Swing Check Valve Weld Ends Carbon Steel with
Anti-Rotating Disc
Nine Mile Point Nuclear Station Unit 2 Calculation No. A10.1-E-116, Air Leakage Rate to Water
Leakage Rate Correlation
Wylie Laboratories, Wylie Certification Test Report No. 17761-1, report prepared for Public
Service Electric & Gas Company, Hope Creek Generating Station, Hancocks Bridge, NJ,
November 6, 1983
FWS*V23B
FWS*23B hinge pin cover found during steam tunnel walkdown
O1-OPS-001-215-1-02, Neutron Monitoring System
O1-OPS-001-212-1-01, Reactor Protection System
N1-OP-38C, "Local Power Range Monitors (LPRM) Average Power Range Monitors"
A-7AttachmentSection 1R19: Post Maintenance TestingWO 06-11287-00WO 07-01313-00
WO 05-02332-00
WO 05-01272-00
ACR 06-5782
N2-ISP-RPS-R211, "Channel Scram Response Time Test"
N2-OSP-RPS-W002, "Manual Scram Channel Functional Test"
N2-OSP-SWP-Q002, "Service Water Pump and Valve Operability Test"
N2-OSP-SWP-Q004, "Division 2 Service Water Operability Test"
N2-OSP-RHS-Q003, "RHR System Loop C Valve Operability Test"
MAI-01, "Conduct of Maintenance"
N1-ST-R11, "Valve Remote Position Indicator Verification" completed January 24, 2007
N1-ST-SA6, "Drywell/Torus and Torus/RB Vacuum Reliefs Test" completed January 24, 2007
N1-MMP-068-251, "Maintenance of Containment Vacuum Relief Valves"
N1-PM-W9, "Fire Protection System - Weekly Operation of Fire Pumps" completed January 26,
2007
N1-MPM-100-851, "Diesel Fire Pump Engine Preventative Maintenance"
N2-ISP-LRT-R@102, "Type "C" Containment Isolation Valve Vacuum Leak Rate Test
FWS*V23B" completed on March 12, 2007
N2-IPM-LRT-@001, "Leak rate Monitor Flow and Electrical Integrity Check"
N2-OP-3, "Condensate and Feedwater System"Section 1R20: Refueling and Outage ActivitiesCNG-HU-1.01, "Human Performance Program"CNG-HU-1.01-1000, "Human Performance"
OPS-117, "Integrated Risk Management"
S-RPIP-10.4, "Primary Containment Entries"
N1-FHP-27C, "Core Shuffle"
N1-FHP-25, "General Description of Fuel Moves"
N1-ODP-NFM-101, "Refueling Operations"
N1-ODP-OPS-0108, "Shutdown Operations Protection"
N1-OP-34, "Refueling Procedure"
N1-OP-43C, "Plant Shutdown"
N1-OP-4, "Shutdown Cooling System"
N2-OP-101C, "Plant Shutdown"
N2-OP-101A, "Plant Start-up"
N2-OSP-RCS-@001, "RCS Pressure/Temperature Verification"
A-8AttachmentSection 1R22: Surveillance TestingN2-ISP-LDS-Q007, "Quarterly Functional Test of
TE49C, and2RHS*TE49D"
N1-ST-Q6C, "Containment Spray System Loop 112 Quarterly Operability Test"
N2-OSP-RHS-Q@006, "RHR System Loop C Pump and Valve Operability Test and System
Integrated Test"
N1-ST-Q1B, "CS [Core Spray] 121 Pump, Valve and SDC [Shutdown Cooling] Water Seal
Check Valve Operability Test"
N1-ST-R9, "Core Spray Operability Test Using Demineralized (CST) Water"
VAC-DG-ES, D.G. Loading
N1-ST-M4A, "EDG 102 and PB 102 Operability Test" completed on January 22, 2007
N1-OP-33A, "115 kV System"
N2-OSP-CSH-Q@002, "HPCS Pump and Valve Operability and System Integrity Test"
completed on January 25, 2007
N2-OP-100B, "HPCS Diesel Generator"
N2-OSP-EGS-M@002, "Diesel Generator and Diesel Air Start Valve Operability Test - Division
- AS [[]]
ME Code Class 1and 2 Components"
ACR 06-06587, Hinge Pin cover leaking approximately 100 drops per minute
Design Change Package (DCP) No. N2-01-203, Check Valve Internals Modification
AOV23A/B
Dwg No. 0005360170408, 24 inch, 900 lb., Swing Check Valve Weld Ends Carbon Steel with
Anti-Rotating Disc
Nine Mile Point Nuclear Station Unit 2 Calculation No. A10.1-E-116, Air Leakage Rate to Water
Leakage Rate Correlation
Wylie Laboratories, Wylie Certification Test Report No. 17761-1, report prepared for Public
Service Electric & Gas Company, Hope Creek Generating Station, Hancocks Bridge, NJ,
November 6, 1983
FWS*V23B
FWS*23B hinge pin cover found during steam tunnel walkdown
A-9AttachmentSection
HU-1.01-1001, "Human Performance Tools and Verification Practices"
S-ODP-OPS-0001, "Conduct of Operations"
EPP-20, "Emergency Notifications"
Emergency Preparedness Scenario for the
OA2: Identification and Resolution of ProblemsCondition Reports2004-00102006-0014
2007-0512
2004-4736
2006-4881
2004-4977
2005-1494
2007-1464
2007-1540
2003-1306
2003-1064
2007-1477
2007-1695
2007-1905
2007-1786
2007-0181
2007-0421
2007-0392
2007-02112007-08382007-0869
2007-0870
2007-1090
2007-0393
2007-0547
2007-1179
2007-1181
2007-0236
2007-0358
2007-1821
2006-3145
2007-0558
2007-1403
2007-0547
2007-0480
2007-0181
2007-0311
2006-58832006-58772007-0052
2007-0011
2006-5855
2006-0026
2007-0355
2007-0414
2007-0430
2007-0448
2007-0552
2007-0625
2007-0653
2007-0667
2007-0730
2007-0722
2007-0727
2007-0838
2007-08692007-09002007-1179
2007-1187
2007-1180
2007-1192
2007-1181
2007-1191
2007-1059
2007-1100
2007-0948
2007-0962
2007-1208
2007-1370
2007-1405
2007-1574
2007-1540
2007-1464Section
OGESMS Alternate Monitoring Plan
N2-SOP-29.1, "RRP Seal Failure"
N2-SOP-29, "Sudden Reduction in Core Flow"
RCS leakage rate
A-10AttachmentLIST
- OF [[]]
ACRONYMSADAMSAgencywide Document and Management SystemASMEAmerican Society of Mechanical Engineers
CAPcorrective action program
CRcondition report
DBDdesign basis documents
ECemergency cooling system
EDGemergency diesel generator
- GT [[]]
AWgas tungsten arc welding
- IPE [[]]
EEindividual plant examination of external events
ISIinservice inspection
kVkilovolt
- LO [[]]
RTlicensed operator requalification training
MTmagnetic particle test
MRmaintenance rule
NCVsnon-cited violations
- NMPN [[]]
- NR [[]]
- OD [[]]
- OGES [[]]
MSoff-gas effluent stack monitoring system
- PA [[]]
RSpublicly available records
PQRprocedure qualification record
PRAprobabilistic risk assessment
PTpenetration test
- RBC [[]]
- RC [[]]
ICreactor core isolation cooling
RHRresidual heat removal
RPVreactor pressure vessel
- RW [[]]
CUreactor water clean up
- SM [[]]
- SP [[]]
- SR [[]]
ASenior Reactor Analyst
SSCstructures, systems, or components
STsurveillance test
TCPtemporary change packages
- UFSA [[]]
RUpdated Final Safety Evaluation Report
UTultrasonic test
Vdcvolts direct current
VTvisual examination