IR 05000382/2016003

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NRC Integrated Inspection Report 05000382/2016003
ML16315A149
Person / Time
Site: Waterford Entergy icon.png
Issue date: 11/10/2016
From: Geoffrey Miller
NRC/RGN-IV/DRP/RPB-D
To: Chisum M
Entergy Operations
GEOFF MILLER
References
IR 2016003
Download: ML16315A149 (37)


Text

UNITED STATES ber 10, 2016

SUBJECT:

WATERFORD STEAM ELECTRIC STATION, UNIT 3 - NRC INTEGRATED INSPECTION REPORT 05000382/2016003

Dear Mr. Chisum:

On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Waterford Steam Electric Station, Unit 3. On October 13, 2016, the NRC inspectors discussed the results of this inspection with Mr. D. Brenton and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements. Further, inspectors documented a licensee-identified violation which was determined to be of Severity Level IV in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Waterford Steam Electric Station, Unit 3. In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Geoffrey Miller, Branch Chief Projects Branch D Division of Reactor Projects Docket No. 50-382 License No. NPF-38

Enclosure:

Inspection Report 05000382/2016003 w/ Attachment 1: Supplemental Information Attachment 2: O

REGION IV==

Docket: 05000382 License: NPF-38 Report: 05000382/2016003 Licensee: Entergy Operations, Inc.

Facility: Waterford Steam Electric Station, Unit 3 Location: 17265 River Road Killona, LA 70057 Dates: July 1 through September 30, 2016 Inspectors: F. Ramírez, Senior Resident Inspector C. Speer, Resident Inspector A. Barret, Resident Inspector B. Parks, Project Engineer C. Steely, Operations Engineer M. Phalen, Senior Health Physicist G. Guerra, Health Physicist S. Money, Health Physicist, Accompaniment Approved By: Geoffrey Miller Chief, Projects Branch D Division of Reactor Projects-1- Enclosure

SUMMARY

IR 05000382/2016003; 07/01/2016 - 09/30/2016, Waterford Steam Electric Station, Unit 3;

Maintenance Effectiveness.

The inspection activities described in this report were performed between July 1 and September 30, 2016, by the resident inspectors at Waterford Steam Electric Station, Unit 3, and inspectors from the NRCs Region IV office. One finding of very low safety significance (Green)is documented in this report. This finding involved a violation of NRC requirements.

Additionally, NRC inspectors documented in this report one licensee-identified violation of Severity Level IV. The significance of inspection findings is indicated by their color (Green,

White, Yellow, or Red), which is determined using Inspection Manual Chapter 0609,

Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.

Cornerstone: Mitigating Systems

Green.

The inspectors reviewed a self-revealing, Green, non-cited violation of Technical Specification 6.8, Procedures and Programs, associated with the licensees failure to perform maintenance that could affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Specifically, on March 5, 2013, the licensee used a procedure that did not contain sufficient detail for reassembly of an actuator for a safety-related auxiliary component cooling water valve. As a result, on June 27, 2016, the lower clevis fastener bolt for ACC-126A, the safety-related valve, failed and it was consequently declared inoperable.

The licensee entered this issue into their corrective action program as condition report CR-WF3-2016-04209. The corrective action taken to restore compliance was to reassemble the lower clevis fastener bolt of ACC-126A appropriately and restore the safety-related valve to service.

The inspectors concluded that the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to ensure proper installation of the lower clevis fastener bolt for the actuator associated with ACC-126A resulted in its subsequent inoperability. The inspectors used NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Findings At-Power, to determine the significance of the finding. The inspectors determined that the finding required a detailed risk evaluation because it represented the actual loss of a function for greater than its allowed technical specification outage time. This condition was assumed to not challenge the availability of sufficient inventory in the wet cooling tower for the mission time required for operators to attain safe and stable plant conditions. From this the senior reactor analyst determined that the finding was of very low safety significance (Green) when evaluating any increase in core damage frequency. The analyst used NRC Inspection Manual Chapter 0609, Appendix H,

Containment Integrity Significance Determination Process, dated May 6, 2004, to determine that since the finding did not contribute directly to a steam generator tube rupture or an intersystem loss of coolant accident, the condition did not represent a significant increase in large early release frequency. Because the performance deficiency occurred in 2013, and a specific procedure for the work has since been created, the inspectors concluded that the finding does not reflect current licensee performance and therefore did not assign a cross-cutting aspect. (Section 1R12)

=

Licensee-Identified Violations===

A Severity Level IV violation that was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and associated corrective action tracking numbers are listed in Section 4OA7 of this report.

PLANT STATUS

The Waterford Steam Electric Station, Unit 3, began the inspection period at 100 percent power.

On July 2, 2016, an unexpected closure of valves associated with feedwater heaters resulted in operators reducing plant power to 73 percent. Following repairs to the valves, the operators increased power the following day and achieved 100 percent power on July 4, 2016. The unit remained at full power for the remainder of the inspection period.

REPORT DETAILS

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

On August 26, 2016, the inspectors completed an inspection of the stations readiness for impending adverse weather conditions. The inspectors reviewed plant design features, the licensees procedures to respond to pending hurricane landfall, and the licensees implementation of these procedures. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant.

These activities constituted one sample of readiness for impending adverse weather conditions, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walk-Down

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant systems:

  • On August 26, 2016, essential chilled water train A with trains B and AB out of service for emergent maintenance
  • On September 22, 2016, fuel pool cooling following maintenance The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constituted three partial system walk-down samples as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

.2 Complete Walk-Down

a. Inspection Scope

On August 18, 2016, the inspectors performed a complete system walk-down inspection of the high pressure safety injection system. The inspectors reviewed the licensees procedures and system design information to determine the correct high pressure safety injection system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, open condition reports, and other open items tracked by the licensees operations and engineering departments. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.

These activities constituted one complete system walk-down sample, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on five plant areas important to safety:

  • On July 30, 2016, fire area RAB 36, safety injection pump room A
  • On July 30, 2016, fire area NS-TB-001, turbine building +15 east
  • On August 19, 2016, fire area RAB 8C, switchgear room A/B
  • On August 19, 2016, fire area RAB 12, battery room AB
  • On August 26, 2016, fire area RAB 2, heating and ventilation mechanical room For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constituted five quarterly inspection samples, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

.2 Annual Inspection

a. Inspection Scope

On September 26, 2016, the inspectors completed their annual evaluation of the licensees fire brigade performance. This evaluation included observation of an unannounced fire drill in fire area 24, decon area, on September 24, 2016.

During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigades use of turnout gear and fire-fighting equipment, and the effectiveness of the fire brigades team operation. The inspectors also reviewed whether the licensees fire brigade met NRC requirements for training, dedicated size and membership, and equipment.

These activities constituted one annual inspection sample, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

a. Inspection Scope

On August 15, 2016, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors verified the licensee used the industry standard periodic maintenance method outlined in EPRI NP-7552 for the essential chillers. Additionally, the inspectors walked down the essential chillers to observe its performance and material condition and verified that the essential chillers were correctly categorized under the Maintenance Rule and were receiving the required maintenance.

These activities constituted completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On August 2, 2016, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance.

These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

The inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity or risk. The inspectors observed the operators performance of the following activities:

  • On September 15, 2016, heightened activity due to main feed regulating valve A maintenance
  • On September 29 and September 30, 2016, heightened activity due to maintenance on the core protection calculator C, and system testing In addition, the inspectors assessed shift communications, response to expected alarms, switch manipulations, and the operators adherence to plant procedures, including conduct of operations procedure and other operations department policies.

These activities constituted completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.3 Annual Review of Requalification Examination Results

The licensed operator requalification program involves two training cycles that are conducted over a two-year period. In the first cycle, the annual cycle, the operators are administered an operating test consisting of job performance measures and simulator scenarios. In the second part of the training cycle, the biennial cycle, operators are administered an operating test and a comprehensive written examination. For this annual inspection requirement the licensee was in the first part of the training cycle.

a. Inspection Scope

The inspectors reviewed the results of the operating tests to satisfy the annual requirements.

On August 30, 2016, the licensee informed the inspectors of the following results:

  • 8 of 8 crews passed the simulator portion of the operating test
  • 51 of 51 licensed operators passed the simulator portion of the operating test

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed two instances of degraded performance or condition of safety-related structures, systems, and components (SSCs):

  • On July 27, 2016, auxiliary component cooling water system
  • On August 16, 2016, wet cooling tower chemical addition and filtration skids The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constituted completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.

b. Findings

Introduction.

The inspectors reviewed a self-revealing, Green, non-cited violation of Technical Specification 6.8, Procedures and Programs, associated with the licensees failure to perform maintenance that could affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Specifically, on March 5, 2013, the licensee used a procedure that did not contain sufficient detail for reassembly of an actuator for a safety-related auxiliary component cooling water valve that resulted in the valves inoperability on June 27, 2016.

Description.

On June 27, 2016, the licensee performed a quarterly test of the auxiliary component cooling water header A component cooling water heat exchanger outlet temperature control valve (ACC-126A). During the test, ACC-126A failed in the as-is position when operators attempted to stroke the valve. The valve was declared inoperable and, during troubleshooting, the licensee discovered the lower clevis bolt had dislodged from the assembly connecting the actuator to the valve. Due to the dislodged bolt, the actuator could not change the position of the valve. The licensee connected the actuator to the valve in accordance with design drawings and returned ACC-126A to an operable status on June 28, 2016. The licensee previously performed successful quarterly testing of ACC-126A on March 28, 2016. Prior to the failure, the valve was in service as of May 24, 2016, with no notable degradation in performance until its failure during the June 27, 2016, surveillance test.

In reviewing the issue, the licensee found that maintenance affecting the lower clevis bolt was last performed on March 5, 2013. At that time, specific procedures for the assembly of the ACC-126A valve actuator did not exist. Due to obstructions near the valve, personnel performing the work could not see if the lower clevis connection between the actuator and valve was reassembled appropriately. Additionally, work order instructions did not include guidance to ensure that personnel were aware of the appropriate reassembly of the connection. Due to the inappropriate reassembly of the lower clevis bolt connection, over time the actuator and valve connection for ACC-126A loosened and ultimately failed, leading to the June 27, 2016, failure of the valve.

In their review of the event, the inspectors noted that in condition report CR-WF3-2013-1261, the licensee identified that specific procedures did not exist for working on air operated valves, such as ACC-126A. One of the corrective actions of that condition report included the creation of procedure MM-006-132, ACCMVAA126-A and ACC Header CCW HX OUTL TEMP CNTR Valve and CC MCAA620, Fuel Pool Heat EXCHs Temperature Control Disassembly, Inspection and Reassembly, in order to provide specific instructions for the disassembly and reassembly of the valve and actuator for ACC-126A. However, that procedure was not approved until November 11, 2014. Since its implementation, MM-006-132 had not been used to work on the lower actuator clevis connection of the ACC-126A valve actuator.

Analysis.

The failure to perform maintenance that could affect the performance of safety-related equipment in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances consistent with Regulatory Guide 1.33, Quality Assurance Program Requirements, as required by Technical Specification 6.8, Procedures and Programs, was a performance deficiency. The performance deficiency was more than minor, and therefore is a finding, because it was associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to ensure proper installation of the lower clevis fastener bolt for the actuator associated with ACC-126A resulted in its subsequent inoperability.

The inspectors used NRC Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, to evaluate the finding for its impact on the Mitigating Systems cornerstone. The initial screening directed the inspectors to use Appendix A, The Significance Determination Process for Findings At-Power, to determine the significance of the finding. Using Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined that the finding required a detailed risk evaluation because it represented the actual loss of a function for greater than its allowed technical specification outage time.

A senior reactor analyst performed a qualitative detailed risk evaluation for this issue.

Valve ACC-126A failed in an intermediate position, which would provide more cooling flow than assumed in plant analyses. Increased flow through Valve ACC-126A above that of its designed accident condition flow would challenge the valves ability to maintain the seven-day, post-accident wet cooling tower inventory for use during events. This condition was assumed to not challenge the availability of sufficient inventory in the wet cooling tower for the mission time required for operators to attain safe and stable plant conditions. From this the analyst determined that the finding was of very low safety significance (Green) when evaluating any increase in core damage frequency. The analyst used NRC Inspection Manual Chapter 0609, Appendix H, Containment Integrity Significance Determination Process, dated May 6, 2004, to determine that since the finding did not contribute directly to a steam generator tube rupture or an intersystem loss of coolant accident, the condition did not represent a significant increase in large early release frequency.

The inspectors determined that the finding did not have a cross-cutting aspect because the most significant contributor to the performance deficiency occurred more than two years ago and did not reflect current licensee performance. Specifically, because the performance deficiency occurred in 2013, and a specific procedure for the work has since been created, the inspectors concluded that the finding does not reflect current licensee performance and therefore did not assign a cross-cutting aspect.

Enforcement.

Technical Specification 6.8, Procedures and Programs, Section 1.a, requires, in part, that procedures shall be established, implemented and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Section 9.a of Regulatory Guide 1.33, Revision 2, Appendix A, requires, in part, that maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to the above, on March 5, 2013, the licensee did not ensure that maintenance that can affect the performance of safety-related equipment was performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Specifically, the licensee used a procedure that did not contain sufficient detail for reassembly of the valve air actuator lower clevis fastener bolt for ACC-12A, a safety-related valve. As a result, on June 27, 2016, the lower clevis fastener bolt for ACC-126A failed and the valve was consequently declared inoperable.

The licensee entered this condition into their corrective action program as Condition Report CR-WF3-2016-04209. The corrective action taken to restore compliance was to reassemble the lower clevis fastener bolt of ACC-126A appropriately and restore ACC-126A to service. A long-term corrective action was to add additional detail to ME-006-132 to ensure proper assembly and disassembly of the actuator associated with ACC-126A in the future.

Because this violation was of very low safety significance and the licensee entered the issue into their corrective action program, this violation is treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy: NCV 05000382/2016003-01, Inadequate Procedure for Assembling a Safety-Related Valve Actuator.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed one risk assessment performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:

  • On August 26, 2016, planned yellow risk due to switchgear ventilation air handling unit AH-30 maintenance, and essential chiller B restoration The inspectors verified that this risk assessment was performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessment and verified that the licensee implemented appropriate risk management actions based on the result of the assessment.

The inspectors also observed portions of four emergent work activities that had the potential to cause an initiating event, or to affect the functional capability of mitigating systems, or to impact barrier integrity:

  • On August 3, 2016, emergent yellow risk due to a tornado warning in the plant area
  • On August 12, 2016, emergent yellow risk due to the failure of essential chiller train A
  • On August 27, 2016, emergent orange risk due to securing power to Emergency Feedwater Pump AB
  • On September 21, 2016, emergent work on charging pump B The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.

These activities constituted completion of five maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed four operability determinations that the licensee performed for degraded or nonconforming SSCs:

  • On August 23, 2016, operability determination of feedwater snubbers FWSR-34 and FWSR-36 The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.
  • From August 23 to September 9, 2016, the inspectors also reviewed operator actions taken or planned to compensate for degraded or nonconforming conditions. The inspectors verified that the licensee effectively managed these operator workarounds to prevent adverse effects on the function of mitigating systems and to minimize their impact on the operators ability to implement abnormal and emergency operating procedures.

These activities constituted completion of five operability and functionality review samples, which included one operator work-around sample, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1R18 Plant Modifications

Permanent Modifications

a. Inspection Scope

On July 12, 2016, the inspectors reviewed a permanent modification to the plant ultimate heat sink. The inspectors reviewed the design and implementation of the modification.

The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the SSC as modified.

These activities constituted completion of one sample of permanent modifications, as defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed seven post-maintenance testing activities that affected risk-significant SSCs:

  • On July 19, 2016, component cooling water pump AB
  • On August 26, 2016, essential chiller train B
  • On August 29, 2016, emergency feedwater pump AB steam supply inlet valve
  • On September 21, 2016, fuel pool heat exchanger temperature control valve The inspectors reviewed licensing- and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constituted completion of seven post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed five risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:

In-service tests:

  • On August 4, 2016, high pressure safety injection pump train A testing Other surveillance tests:
  • On July 20, 2016, safety injection signal actuation testing
  • On August 2, 2016, undervoltage relay testing on safety train A
  • On August 29, 2016, emergency diesel generator A The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constituted completion of five surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on August 31, 2016, to verify the adequacy and capability of the licensees assessment of drill performance. The inspectors reviewed the drill scenario, observed the drill from the control room simulator, and Technical Support Center, and attended the post-drill critique. The inspectors verified that the licensees emergency classifications, off-site notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.

These activities constituted completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

2.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS2 Occupational ALARA Planning and Controls

a. Inspection Scope

The inspectors assessed licensee performance with respect to maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors performed this portion of the attachment as a post-outage review. During the inspection the inspectors interviewed licensee personnel, reviewed licensee documents, and evaluated licensee performance in the following areas:

  • Radiological work planning, including work activities of exposure significance, and radiological work planning ALARA evaluations, initial and revised exposure estimates, and exposure mitigation requirements. The inspectors also verified that the licensees planning identified appropriate dose reduction techniques, reviewed any inconsistencies between intended and actual work activity doses, and determined if post-job (work activity) reviews were conducted to identify lessons learned.
  • Verification of dose estimates and exposure tracking systems, including the basis for exposure estimates, and measures to track, trend, and if necessary reduce occupational doses for ongoing work activities. The inspectors evaluated the licensees method for adjusting exposure estimates and reviewed the licensees evaluations of inconsistent or incongruent results from the licensees intended radiological outcomes.
  • Problem identification and resolution for ALARA planning. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of two of the five required samples of occupational ALARA planning and controls program, as defined in Inspection Procedure 71124.02.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment

a. Inspection Scope

The inspectors evaluated the accuracy and operability of the licensees personnel monitoring equipment, verified the accuracy and effectiveness of the licensees methods for determining total effective dose equivalent, and verified that the licensee was appropriately monitoring occupational dose. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:

  • Source term characterization, including characterization of radiation types and energies, hard-to-detect isotopes, and scaling factors.
  • External dosimetry including National Voluntary Laboratory Accreditation Program (NVLAP) accreditation, storage, issue, use, and processing of active and passive dosimeters.
  • Internal dosimetry, including the licensees use of whole body counting, use of in vitro bioassay methods, dose assessments based on airborne monitoring, and the adequacy of internal dose assessments.
  • Special dosimetric situations, including declared pregnant workers, dosimeter placement and assessment of effective dose equivalent for external exposures (EDEX), shallow dose equivalent, and neutron dose assessment.
  • Problem identification and resolution for occupational dose assessment. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the five required samples of occupational dose assessment program, as defined in Inspection Procedure 71124.04.

b. Findings

No findings were identified.

4.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Mitigating Systems Performance Index: Heat Removal Systems (MS08)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of July 1, 2015, through June 30, 2016, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for heat removal systems for Waterford Steam Electric Station, Unit 3, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index: Residual Heat Removal Systems (MS09)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of July 1, 2015, through June 30, 2016, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for residual heat removal systems for Waterford Steam Electric Station, Unit 3, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index: Cooling Water Support Systems (MS10)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of July 1, 2015, through June 30, 2016, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for cooling water support systems for Waterford Steam Electric Station, Unit 3, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

On September 27, 2016, the inspectors reviewed the licensees retraction of Licensee Event Report (LER) 2015-006-00, regarding voids discovered in low pressure safety injection system piping. On June 20, 2015, the licensee discovered voiding in train B of the low pressure safety injection system piping that exceeded the allowable volume.

Prior to the discovery of the void, a filling and venting of the low pressure safety injection system train B occurred on June 9, 2015. Assuming that the void was introduced at the time, the licensee submitted the LER due to exceeding the system technical specification allowed outage time of seven days.

In May of 2016, the licensee completed an evaluation demonstrating that the allowable value used to determine system inoperability was overly conservative. Per the evaluation, the licensee determined that the void discovered on June 20, 2015, was not sufficient to render train B of the low pressure safety injection system inoperable and retracted LER 2015-006-00. The inspectors determined the licensees retraction of LER 2015-006-00 was appropriate.

The inspectors reviewed the licensees cause analyses, and verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to ensure the resolution of the issue.

These activities constituted completion of one annual follow-up sample as defined in Inspection Procedure 71152.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On September 7, 2016, the inspectors presented the licensed operator requalification inspection results to Mr. R. Simpson, Operations Training Superintendent. The inspector did not review any proprietary information during this inspection.

On October 7, 2016, the inspectors presented the radiation safety inspection results by teleconference to Mr. B. Lanka, Director, Engineering, and other members of the licensee staff.

The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On October 13, 2016, the resident inspectors presented the inspection results to Mr. D. Brenton, General Manager, Plant Operations, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

4OA7 Licensee-Identified Violations

The following licensee-identified violation of NRC requirements was determined to be of very low safety significance or Severity Level IV and meets the NRC Enforcement Policy criteria for being dispositioned as a Non-Cited Violation.

  • Title 10 CFR 50.72, Immediate notification requirements for operating nuclear power reactors, section (b)(3)(v), requires, in part, that the licensee shall notify the NRC as soon as practical and in all cases within eight hours of the occurrence of any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (A) shut down the reactor and maintain it in a safe condition; (B) remove residual heat; (C) control the release of radioactive material; or (D)mitigate the consequences of an accident. Contrary to the above, on August 12, 2016, the licensee experienced a loss of the essential chilled services water safety function, which is needed to mitigate the consequences of an accident, and did not notify the NRC within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. The licensee identified this issue and entered it into their corrective action program as CR-WF3-2016-05188 and made the required notification on August 15, 2016. This violation was assessed using Section 2.2.4 of the NRCs Enforcement Policy, revised February 4, 2015. Using the example listed in Section 6.9.d.9, A licensee fails to make a report required by 10 CFR 50.72, the issue was determined to be a Severity Level IV violation.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

D. Brenton, General Manager, Plant Operations
D. Burnett, Corporate Director, Emergency Preparedness, Entergy South
M. Chisum, Site Vice President
J. Clavelle, Manager, Systems and Components
S. Fontenot, Manager, Performance Improvement
R. Gilmore, Director, Regulatory and Performance Improvement
A. Hall, Operations Instructor
A. James, Manager, Security
J. Jarrell, Manager, Regulatory Assurance
B. Lanka, Director, Engineering
R. Ledet, Manager, Operations Support
W. McKinney, Manager, Training
S. Meiklejohn, Senior Licensing Specialist
S. Nelson, Fire Marshall
B. Pellegrin, Manager, Production
P. Rodrigue, Manager Operations
D. Selig, Senior Manager, Maintenance
J. Signorelli, Manager, Emergency Preparedness
R. Simpson, Operations Training Superintendent

NRC Personnel

R. Deese, Senior Reactor Analyst

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000382/2016003-01 NCV Inadequate Procedure for Assembling a Safety-Related Valve

Actuator (Section 1R12)

LIST OF DOCUMENTS REVIEWED