IR 05000397/2006005
| ML070450252 | |
| Person / Time | |
|---|---|
| Site: | Columbia |
| Issue date: | 02/13/2007 |
| From: | Clay Johnson NRC/RGN-IV/DRP/RPB-A |
| To: | Parrish J Energy Northwest |
| References | |
| IR-06-005 | |
| Download: ML070450252 (44) | |
Text
ary 13, 2007
SUBJECT:
COLUMBIA GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000397/2006005
Dear Mr. Parrish:
On December 31, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Columbia Generating Station. The enclosed inspection report documents the inspection findings which were discussed on January 11, 2007, with Mr. Atkinson and other members of your staff.
The inspections examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
This report documents two NRC-identified findings and one self-revealing finding of very low risk significance (Green). All of the findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as noncited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Columbia Generating Station.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document
Energy Northwest -2-Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Claude E. Johnson, Chief Project Branch A Division of Reactor Projects Docket: 50-397 License: NPF-21
Enclosure:
NRC Inspection Report 05000397/2006005 w/Attachment: Supplemental Information
REGION IV==
Docket: 50-397 License: NPF-21 Report: 05000397/2006005 Licensee: Energy Northwest Facility: Columbia Generating Station Location: Richland, Washington Dates: October 1 through December 31, 2006 Inspectors: Z. Dunham, Senior Resident Inspector, Project Branch A, DRP R. Cohen, Temporary Senior Resident Inspector, Project Branch A, DRP J. Drake, Operations Engineer, Operations Branch F. Brush, Senior Project Engineer K. Clayton, Operations Engineer P. Elkmann, Emergency Preparedness Inspector M. Murphy, Senior Operations Engineer C. Paulk, Senior Reactor Inspector, Engineering Branch 1 J. Nadel, Reactor Inspector, Engineering Branch 1 E. Owen, Reactor Inspector, Engineering Branch 1 Accompanying J. Bashore, Project Engineer Personnel Approved By: C. E. Johnson, Chief, Project Branch A, Division of Reactor Projects ATTACHMENT: SUPPLEMENTAL INFORMATION Enclosure
SUMMARY OF FINDINGS
IR05000397/2006005; 10/1/2006 - 12/31/2006; Columbia Generating Station; Surveillance
Testing; Identification and Resolution of Problems; Other Activities The report covered a 13-week period of inspection by resident and regional inspectors. Three Green noncited violations were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
NRC Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
- Green.
A Green self-revealing noncited violation (NCV) of Technical Specification 5.4.1.a was identified for the failure to follow a diesel generator surveillance test procedure. This resulted in the unintentional inoperability of the backup transformer. Energy Northwest entered the issue into their corrective action program for evaluation and resolution.
This finding was more than minor because it had an attribute of human performance which affected the mitigating systems cornerstone objective to ensure the availability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low risk significance (Green) because the backup transformer was inoperable for less than its technical specification allowed outage time. Additionally, the finding was not a qualification issue confirmed not to result in loss of operability, did not represent a loss of safety function, and did not screen as potentially risk significant due to external events. The cause of the finding is also related to the crosscutting aspect of human performance with a work practices causal factor in that self and peer-checking techniques were not implemented properly during the conduct of the test procedure.
This resulted in the failure to follow procedure. (Section 1R22)
- Green.
A Green NRC identified NCV of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, was identified for failing to promptly identify conditions adverse to quality associated with loss of full environmental qualification of plant components due to degraded flexible electrical conduit jackets. Energy Northwest entered the issue into their corrective action program and took immediate action to repair the identified degraded conduit jackets and to plan additional periodic plant walkdowns to identify additional degraded conduit jackets.
The finding was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to preclude undesirable consequences (i.e., core damage). The finding was determined to be of very low safety significance (Green)because although the qualification for high energy line break was affected for some components, the finding did not result in inoperability of any equipment. Additionally, the finding did not represent a loss of safety function, and did not screen as potentially risk significant due to external events. This finding had a crosscutting aspect associated with problem identification and resolution with a corrective action program causal factor.
Specifically, Energy Northwest failed to assess and trend information from the corrective action program in the aggregate resulting in the failure to identify an adverse trend regarding flexible electrical conduit jackets. (Section 4OA2.5)
- Green.
A Green NRC identified NCV of Technical Specification 5.4.1.a was identified for the failure to provide an adequate procedure for alternate boron injection.
Specifically, Emergency Support Procedure 5.5.8, Alternate Boron Injection,
Revision 8, failed to direct venting of a temporarily installed hose between the standby liquid control boron storage tank and the reactor core isolation cooling pump suction. As a result, degraded reactor core isolation cooling pump performance could occur.
Energy Northwest entered the issue into their corrective action program and revised the procedure to vent the hose.
This finding was more than minor because the finding had an attribute of procedure quality which affected the mitigating systems cornerstone objective to ensure the availability and reliability of systems that respond to initiating events to prevent undesirable consequences. The finding was of very low risk significance (Green)because although degraded reactor core isolation cooling pump performance could occur, the pump was expected to perform adequately to support alternate boron injection, based on Energy Northwests engineering evaluation. Additionally, the finding was not a qualification issue confirmed not to result in loss of operability, did not represent a loss of safety function for a single train or for the system, and did not screen as potentially risk significant due to external events.
Licensee Identified Violations
None.
REPORT DETAILS
Summary of Plant Status:
The inspection period began with Columbia Generating Station at 100 percent power. The plant was shutdown following an automatic reactor scram on October 31, 2006, from 100 percent power and entered forced outage F-06-01 due to a failure of a circuit card in the main turbine digital electro hydraulic control system. The reactor plant was brought critical on November 6, 2006, and was synchronized with the grid to end the forced outage on November 8, 2006. The facility operated at 100 percent power with the exception of scheduled reductions in power to support testing for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather
a. Inspection Scope
On October 30, 2006, the inspectors completed a review of the licensee's readiness of seasonal susceptibilities involving extreme cold and freezing temperatures. The inspectors:
- (1) reviewed plant procedures, the Updated Safety Analysis Report, and Technical Specifications to ensure that operator actions defined in adverse weather procedures maintained the readiness of essential systems;
- (2) walked down portions of safety-related systems to ensure that adverse weather protection features and system lineup were sufficient to support operability, including the ability to perform safe shutdown functions;
- (3) evaluated operator staffing levels to ensure the licensee could maintain the readiness of essential systems required by plant procedures; and
- (4) reviewed the corrective action program to determine if the licensee identified and corrected problems related to adverse weather conditions.
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
1R02 Evaluations of Changes, Tests, or Experiments
a. Inspection Scope
The inspectors reviewed the effectiveness of the licensees implementation of changes to the facility structures, systems, and components; risk-significant normal and emergency operating procedures; test programs; and the Updated Final Safety Analysis Report in accordance with 10 CFR 50.59, "Changes, Tests, and Experiments." The inspectors utilized Inspection Procedure 71111.02, "Evaluation of Changes, Tests, or Experiments," for this inspection.
The procedure specifies five as the minimum sample size of safety evaluations and a combination of 10 applicability determinations and screenings, with the emphasis on screenings.
The inspectors reviewed six safety evaluations performed by the licensee since the last NRC inspection of this area at Columbia Generating Station. The evaluations were reviewed to verify that licensee personnel had appropriately considered the conditions under which the licensee may make changes to the facility or procedures or conduct tests or experiments without prior NRC approval. The inspectors reviewed five licensee-performed applicability determinations and five screenings, in which licensee personnel determined that evaluations were not required, to ensure that the exclusion of a full evaluation was consistent with the requirements of 10 CFR Part 50.59.
Evaluations, screenings, and applicability determinations reviewed are listed in the to this report.
The inspectors reviewed and evaluated a sample of recent licensee condition reports to determine whether the licensee had identified problems related to 10 CFR Part 50.59 evaluations, entered them into the corrective action program, and resolved technical concerns and regulatory requirements. The reviewed condition reports are identified in the Attachment.
The inspection procedure specifies inspector review of a required minimum sample of 5 licensee safety evaluations and 10 applicability determinations and screenings (combined). The inspectors completed review of 6 licensee safety evaluations and 10 applicability determinations and screenings (combined).
b. Findings
No findings of significance were identified.
1R04 Equipment Alignments
.1 Partial Walkdown
a. Inspection Scope
The inspectors:
- (1) walked down portions of the risk important systems listed below and reviewed plant procedures and documents to verify that critical portions of the selected systems were correctly aligned; and
- (2) compared deficiencies identified during the walk down to the licensee's corrective action program to ensure problems were being identified and corrected.
- Division 2 Standby Service Water; November 1, 2006
- Division 2 Emergency Diesel Generator; November 2, 2006
- High Pressure Core Spray; November 10, 2006 The inspectors completed three samples.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
.1 Quarterly Inspection
a. Inspection Scope
The inspectors walked down the plant areas listed below to assess the material condition of active and passive fire protection features and their operational lineup and readiness. The inspectors:
- (1) verified when applicable that transient combustibles and hot work activities were controlled in accordance with plant procedures;
- (2) observed the condition of fire detection devices to verify they remained functional;
- (3) observed fire suppression systems to verify they remained functional;
- (4) verified that fire extinguishers and hose stations were provided at their designated locations and that they were in a satisfactory condition;
- (5) verified that passive fire protection features (electrical raceway barriers, fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems) were in a satisfactory material condition;
- (6) verified when applicable that adequate compensatory measures were established for degraded or inoperable fire protection features; and
- (7) reviewed the corrective action program to determine if the licensee identified and corrected fire protection problems.
- Fire Area R-2; Reactor Building; Primary Containment; October 30, 2006
- Fire Area M-9; Reactor Building; Instrument Rack E-IR-H22/P009 Enclosure; October 30, 2006
- Fire Area M-21; Reactor Building South Valve Room; October 31, 2006
- Fire Area M-73; Reactor Building; Instrument Rack E-IR-73 Enclosure; November 1, 2006
- Fire Area RC-1; General Equipment Area; December 11, 2006
- Fire Area M-27; Reactor Building; E-IR-H22/P027; December 12, 2006 The inspectors completed six samples.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures
.1 Internal Flood Protection
a. Inspection Scope
The inspectors performed the following:
- (1) reviewed the Updated Safety Analysis Report, the flooding analysis, and plant procedures to assess seasonal susceptibilities involving internal flooding;
- (2) reviewed the corrective action program to determine if the licensee identified and corrected flooding problems;
- (3) inspected underground bunkers/manholes to verify the adequacy of
- (a) sump pumps,
- (b) level alarm circuits,
- (c) cable splices subject to submergence, and
- (d) drainage for bunkers/manholes;
- (4) verified that operator actions for coping with flooding can reasonably achieve the desired outcomes; and
- (5) walked down the areas listed below to verify the adequacy of:
- (a) equipment seals located below the floodline,
- (b) floor and wall penetration seals,
- (c) watertight door seals,
- (d) common drain lines and sumps,
- (e) sump pumps, level alarms, and control circuits, and
- (f) temporary or removable flood barriers.
- Reactor Building Elevation 522 ft level which consisted of General Floor Area, Motor Control Center Rooms 410 and 411, Reactor Water Cleanup Pump Rooms 1A and 1B; December 11, 2006 The inspectors completed one sample.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
.1 Quarterly Inspection
a. Inspection Scope
On November 13, 2006, the inspectors observed testing and training of senior reactor operators and reactor operators to identify deficiencies and discrepancies in the training, to assess operator performance, and to assess the evaluator's critique. The training scenario involved a rupture of the fire main in the reactor building which resulted in the loss of the residual heat removal Pumps B and C, a reactor core isolation cooling steam leak, and the failure of various electrical busses to transfer to the startup transformer following a manual reactor scram.
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
.2 Biennial Inspection
a. Inspection Scope
This inspection was held during the week of December 11, 2006, the week before the end of the biennial examination testing cycle. The inspectors reviewed the overall pass/fail results of the individual job performance measure operating tests, simulator operating tests, and written examinations administered by the licensee during the operator licensing requalification biennial examination. Forty-eight licensed operators participated in simulator operating tests, and job performance measure operating tests.
There were two operators who failed portions of the examination, they were remediated and passed the retake examinations. All of the licensed operators tested passed the biennial examination.
The inspectors reviewed biennial examination simulator job performance measures, in-plant job performance measures, the simulator static examination, and written examination. The inspectors also reviewed nine licensed operator annual medical forms and the procedures governing the medical examination process. The inspectors also interviewed two reactor operators, two senior operators, one simulator supervisor, one evaluator, one instructor, one training supervisor and the operations training manager regarding the policies and practices for administering examinations.
The inspectors assessed the Columbia Generating Station plant-referenced simulator for compliance with 10 CFR 55.46 using Baseline Inspection Procedure 71111.11. This assessment included the adequacy of the licensees simulation facility for use in operator licensing examinations and for satisfying experience requirements as prescribed by 10 CFR 55.46. The inspectors reviewed a sample of simulator performance test records (steady state tests, real time tests, transient tests, surveillance tests, core performance tests, and scenario-based tests), simulator discrepancy report records, and processes for ensuring simulator fidelity commensurate with 10 CFR 55.46 and the commitments the licensee had made in implementing ANSI/ANS-3.5 1998. The inspectors assessed the effectiveness of the facility licensees process for continued assurance of simulator fidelity with regard to identifying, reporting, correcting, and resolving simulator discrepancies via a corrective action program. The inspectors confirmed that the simulator has not been used for reactivity manipulation credits for initial license applications. The licensee has scheduled several improvements to the simulator, including core model replacement in late 2007.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed the activities listed below to:
- (1) verify the appropriate handling of structure, system, and component (SSC) performance or condition problems;
- (2) verify the appropriate handling of degraded SSC functional performance;
- (3) evaluate the role of work practices and common cause problems; and
- (4) evaluate the handling of SSC issues reviewed under the requirements of the Maintenance Rule, 10 CFR Part 50 Appendix B, and the Technical Specifications.
- PER 206-0534; EDR-V-19 Drywell Drain Discharge Containment Isolation Valve Declared Inoperable; October 1, 2006
- PER 206-0551; RCIC-V-1 Closed Automatically; October 6, 2006
- PER 206-0585; Procedure step missed in OSP-ELEC-S702 resulting in a possible blown fuse on the Ready to Transfer Light for E-CB-B/8; October 19, 2006 The inspectors completed three samples.
b. Findings
.
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
.1 Risk Assessment and Management of Risk
a. Inspection Scope
The inspectors reviewed the risk assessment activities listed below to verify:
- (1) performance of risk assessments when required by 10 CFR 50.65 (a)(4) and licensee procedures prior to changes in plant configuration for maintenance activities and plant operations;
- (2) the accuracy, adequacy, and completeness of the information considered in the risk assessment;
- (3) that the licensee recognizes, and/or enters as applicable, the appropriate licensee-established risk category according to the risk assessment results and licensee procedures; and
- (4) the licensee identified and corrected problems related to maintenance risk assessments.
- E-CB-DG1/7 Inspection and DG1 Monthly Operability Test; October 2, 2006
- SGT B Maintenance Outage; October 23, 2006
- HPCS-P-2 Outage; October 31 thru November 9, 2006 The inspectors completed four samples.
b. Findings
No findings of significance were identified.
1R17 Permanent Plant Modifications
a. Inspection Scope
The inspection procedure requires inspection of a minimum sample size of five permanent plant modifications.
The inspectors reviewed five permanent plant modification packages and associated documentation, such as implementation reviews, safety evaluation applicability determinations, and screenings, to verify that they were performed in accordance with regulatory requirements and plant procedures. The inspectors also reviewed the procedures governing plant modifications to evaluate the effectiveness of the program for implementing modifications to risk-significant systems, structures, and components, such that these changes did not adversely affect the design and licensing basis of the facility. Procedures and permanent plant modifications reviewed are listed in the to this report. Further, the inspectors interviewed the cognizant design and system engineers for the identified modifications as to their understanding of the modification packages and process.
The inspectors evaluated the effectiveness of the licensees corrective action process to identify and correct problems concerning the performance of permanent plant modifications by reviewing a sample of related condition reports. The reviewed condition reports are identified in the Attachment.
The inspection procedure specifies inspector-review of a required minimum sample of five permanent plant modifications. The inspectors completed review of five permanent plant modifications.
b. Findings
No findings of significance were identified.
1R19 Postmaintenance Testing
a. Inspection Scope
The inspectors selected the postmaintenance test activities of risk significant systems or components listed below for review. For each item, the inspectors:
- (1) reviewed the applicable licensing basis and/or design-basis documents to determine the safety functions;
- (2) evaluated the safety functions that may have been affected by the maintenance activity; and
- (3) reviewed the test procedure to ensure it adequately tested the safety function that may have been affected. The inspectors either witnessed or reviewed test data to verify that acceptance criteria were met, plant impacts were evaluated, test equipment was calibrated, procedures were followed, jumpers were properly controlled, the test data results were complete and accurate, the test equipment was removed, the system was properly re-aligned, and deficiencies during testing were documented. The inspectors also reviewed the corrective action program to determine if the licensee identified and corrected problems related to postmaintenance testing.
- Work Order 01116867; Standby Gas Treatment Relay Replacement; November 28, 2006
- Work Order 01114075; HPCS-P-2 Operability /PMT
- Work Order 01126167; PMT - TDR Testing for IRM-DET-2C Detector Cable, November 3, 2006
- Work Order 01100689; SRM-W403 Channel C CFT, November 3, 2006
- Work Order 01100773; SRM-W402 Channel B CFT, November 3, 2006
- Work Order 01104378; Repair/Replace Limit Switch for MS-V-22D, November 3, 2006
- Work Order 01126133; Replace Failed NDI card Turbine Trip Logic in DEH-CAB-01 Card Slot C1-H-30; November 7, 2006
- Work Order 01121174; Quarterly Battery Testing 250 VDC E-B2-1; Revision 7 The inspectors completed eight samples.
b. Findings
No findings of significance were identified.
1R20 Refueling and Outage Activities
.1 Forced Outage FO-06-01
a. Inspection Scope
The inspectors reviewed the following risk significant outage activities to verify defense in depth commensurate with the outage risk control plan and compliance with the technical specifications:
- (1) the outage risk control plan;
- (2) reactor coolant system instrumentation;
- (3) electrical power;
- (4) decay heat removal;
- (5) heatup and cooldown activities; and
- (6) licensee identification and implementation of appropriate corrective actions associated with refueling and outage activities.
The inspectors completed one sample.
b. Findings
Introduction:
An Unresolved Item (URI) was identified pending the NRCs additional inspection to determine
- (1) if an inadequate procedure caused the problem, and
- (2) determine the risk significance of any performance deficiency associated with the loss of shutdown cooling.
Description:
On November 3, 2006, during a forced outage with shutdown cooling in operation in Mode 4, operators implemented Procedure PPM 2.7.6, Reactor Protection System, Revision 23, to transfer the Reactor Protection System (RPS) B to its alternate power supply to support a maintenance activity. Step 5.9.6 provided the following:
If transferring RPS-B to ALT B or NORMAL, AND maintaining RHR in Shutdown Cooling, THEN VERIFY the disconnects are OPEN for the following valves per SOP-RHR-SDC-BYPASS: Otherwise, N/A.
- RHR-V-8 (RHR-42-S21A7B)
- RHR-V-9 (RHR-DISC-V/9)
- RHR-V-53A (RHR042-7BA5B)
- RHR-V-53B (RHR-42-7BA8C)
The intention of the step was to allow the operating residual heat removal (RHR)
Pump RHR-P-2B to remain running to ensure that shutdown cooling was not interrupted during the transfer. Energy Northwest completed the transfer of RPS B at 3:02 a.m. At 3:09 a.m., shutdown cooling inboard suction Valve, RHR-V-9, disconnect, RHR-DISC-V/9, was closed per PPM 2.7.6, Step 5.9.17. Operators noted that valve RHR-V-9 automatically closed when power was restored to the valve resulting in a trip of pump RHR-P-2B and loss of shutdown cooling. Energy Northwest operators entered ABN-RHR-SDC-LOSS and ABN-LEVEL. Operators removed control power fuses for Pump RHR-P-2B and performed a vent and fill verification per Procedure OSP-RHR-M102. Valve RHR-V-9 logic was reset and the Pump RHR-P-2B breaker was reclosed, restoring shutdown cooling at 3:54 a.m. At the time shutdown cooling was lost, reactor pressure vessel level was + 70 inches with reactor coolant system temperature at 114 °F. At the time that shutdown cooling was restored, operators noted that reactor pressure vessel level had increased to + 95 inches and that reactor coolant system temperature peaked at 148 °F. Operators subsequently restored reactor vessel level and system temperature to the previously maintained operating bands of 60-80 inches and 110-120 °F at 4:51 a.m. However, at the end of the inspection period, additional inspection was needed to determine
- (1) if an inadequate procedure caused the problem, and
- (2) determine the risk significance of any performance deficiency associated with the loss of shutdown cooling. Therefore, pending additional inspection this item will remain open as unresolved item (URI 05000397/2006005-01; Loss of Shutdown Cooling).
Analysis:
A determination of any risk significance associated with any performance deficiencies will be addressed in the resolution of the URI.
Enforcement.
A determination of enforcement aspects associated with any performance deficiencies will be addressed in the resolution of the URI.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the Updated Final Safety Analysis Report, procedure requirements, and Technical Specifications to ensure that the surveillance activities listed below demonstrated that the SSCs tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the following significant surveillance test attributes were adequate:
- (1) preconditioning;
- (2) evaluation of testing impact on the plant;
- (3) acceptance criteria;
- (4) test equipment;
- (5) procedures;
- (6) jumper/lifted lead controls;
- (7) test data;
- (8) testing frequency and method demonstrated Technical Specification operability;
- (9) test equipment removal;
- (10) restoration of plant systems;
- (11) fulfillment of ASME Code requirements;
- (12) updating of performance indicator data;
- (13) engineering evaluations, root causes, and bases for returning tested SSCs not meeting the test acceptance criteria were correct;
- (14) reference setting data; and
- (15) annunciators and alarms setpoints. The inspectors also verified that the licensee identified and implemented any needed corrective actions associated with the surveillance testing.
- OSP-ELEC-S702; Diesel Generator 2 Semi-Annual Operability Test, October 19, 2006
- OSP-INST-H101; Shift and Daily Instrument Checks (Modes 1, 2, 3);
November 30, 2006
- OSP-FPC/IST-Q701; Fuel Pool Cooling System Operability Surveillance, December 6, 2006
- OSP-RRC/IST-Q701; RRC Valve Operability; December 27, 2006 The inspectors completed five samples which included a review of an in-service pump and valve test, a reactor coolant system leak detection surveillance test, and a containment isolation valve surveillance test.
b. Findings
Introduction.
A self-revealing Green noncited violation (NCV) of Technical Specification 5.4.1.a was identified for the failure to adequately implement a surveillance test procedure resulting in the inoperability of the backup transformer. Additionally, a crosscutting aspect in human performance associated with work practices was identified.
Description.
On October 19, 2006, operators performed Procedure OSP-ELEC-S702, Diesel Generator 2 Semi-Annual Operability Test, Revision 26, to conduct a semi-annual surveillance test on diesel generator (DG)-2. In preparation for closing the DG output Breaker E-CB-DG2/8, the test procedure directed placing the CB-DG2/8 Sync
Selector switch to the manual check position and then to adjust DG-2 generator voltage per Step 7.6.23 to slightly higher than SM-8 voltage which was being supplied from the startup Transformer TR-S, through electrical Bus SM-3. The operators noted that the DG-2 output voltage could not be increased enough to raise output voltage greater than SM-8 voltage. The operators noted that the procedure then provided a note as follows:
Note: SM-8 may be paralleled to TR-B per PPM 2.7.1A, provided the following:
Note: The following condition is commonly encountered during an outage when TR-S voltage is high and DG-2 voltage regulator is unable to attain sufficient voltage while unloaded.
DG-2 cannot be paralleled to TR-S (via SM-8) or TR-S is supplying all plant loads in Modes 1, 2, 3.
and SM-7 is not paralleled to TR-B.
The operators determined that Procedure PPM 2.7.1A should be performed to transfer SM-8 to the backup Transformer TR-B, since DG-2 could not be paralleled to TR-S due to known DG-2 voltage limitations. The operators then transitioned to PPM 2.7.1A. The operators failed to note though that the next step of OSP-ELEC-S702, Step 7.6.24(a),directed to first place CB-DG2/8 Sync Selector to Off and then to transfer SM-8 to TR-B per PPM 2.7.1A.
Procedure 2.7.1A, Step 5.12.9, directed placing the CB-B8 Sync Selector switch to manual. The operators noted that following this step that both the CB-DG2/8 Sync Selector and the CB-B8 Sync Selector were in Manual Check and Manual respectively.
Control staff also noted that the E-CB-B8 ready to transfer light was extinguished and incoming voltage was zero. A follow-up investigation by Energy Northwest determined that having both sync selector switches in manual at the same time created a mismatch in voltages to be present in the synchronization circuitry and caused an overcurrent condition which cleared a circuit fuse. As a result, the ready to transfer indication for breaker E-CB-B/8 was de-energized indicating that the breaker was not capable of auto-closure. Energy Northwest declared TR-B inoperable at 11:15 a.m. Energy Northwest subsequently replaced the cleared fuse and declared TR-B operable at 3:52 p.m.
Energy Northwest subsequently identified that the reactor operator and a peer checker failed to adequately implement self and peer-checking techniques which operators are expected to use. As a result, the operator and peer checker failed to evaluate the intended action of placing the CB-B/8 Sync Selector switch to the manual position which would energize the synchronization circuitry. A full review of the procedure step by the operators would have revealed that the synchronization circuitry was already energized with the CB-DG2/8 Synch Selector switch in the manual check position.
Analysis.
The performance deficiency associated with this finding is Energy Northwests failure to properly implement Procedure OSP-ELEC-S702 in accordance with TS 5.4.1.a. resulting in inadvertent inoperability of TR-B. This self-revealing finding was more than minor because the finding had an attribute of human performance which affected the mitigating systems cornerstone objective to ensure the availability of systems that respond to initiating events to prevent undesirable consequences.
Specifically, the failure to follow procedure resulted in inoperability of TR-B. Utilizing NRC Manual Chapter 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, Phase 1 screening, the inspectors determined that the finding was of very low risk significance (Green) because the backup transformer was inoperable for less than its technical specification allowed outage time. Additionally, the finding was not a qualification issue confirmed not to result in loss of operability, did not represent a loss of safety function for a single train or for the system, and did not screen as potentially risk significant due to external events.
This finding had crosscutting aspects in the area of human performance associated with work practices in that self and peer-checking techniques were not implemented properly during the conduct of a safety-related test procedure. This resulted in the failure to follow procedure.
Enforcement.
Technical Specification 5.4.1.a requires in part that written procedures shall be established and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation), Revision 2, Appendix A, Section 8.b.(2)(q) requires that specific surveillance tests should be written for emergency power tests. Contrary to this requirement, on October 19, 2006, operators failed to perform Step 7.6.24(a) of OSP-ELEC-S702 subsequently rendering TR-B inoperable. Because this finding was of very low safety significance and was entered into the licensees corrective action program as PER 206-0584, this violation is being treated as an NCV, consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000397/2006005-02; Failure to Follow Diesel Generator Surveillance Test Procedure). Energy Northwest implemented immediate corrective actions to restore TR-B to an operable condition.
1R23 Temporary Plant Modifications
a. Inspection Scope
The inspectors reviewed the Updated Final Safety Analysis Report, plant drawings, procedure requirements, and Technical Specifications to ensure that the two below listed temporary modifications were properly implemented. The inspectors:
- (1) verified that the modification did not have an affect on system operability/availability;
- (2) verified that the installation was consistent with the modification documents;
- (3) ensured that the post-installation test results were satisfactory and that the impact of the temporary modification on permanently installed SSCs were supported by the test;
- (4) verified that the modifications were identified on control room drawings and that appropriate identification tags were placed on the affected drawings; and
- (5) verified that appropriate safety evaluations were completed. The inspectors verified that the licensee identified and implemented any needed corrective actions associated with temporary modifications.
The inspectors completed one sample.
- Temporary Modification Request 06-002; Install a temporary jumper in the control room termination Cabinet E-CP-H13/P807 due to BS-V-39B staying open and not cycling based on level switch for Trap #17; December 4, 2006
b. Findings
No findings of significance were identified.
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The inspector performed in-office reviews of Revisions 44 and 45 to the Columbia Generating Station Emergency Plan, Revisions 17 and 18 to Emergency Plan Implementing Procedure 13.1.1A, "Classifying the Emergency - Technical Bases," and Revision 35 to Procedure 13.1.1, "Classifying the Emergency," submitted in July and August 2006. These revisions
- (1) described the Security Supervisor position and the Plant Security Force in the emergency plan,
- (2) made changes in Emergency Action Levels 6.1.U.1, 6.1.A.1, 6.1.A.2, 6.1.S.1, 6.2.U.1, 6.2.S.1, and 6.1.G.1, to address installation of crosstie capability between Diesel Generator 3 and Buses SM-7 and -8,
- (3) updated emergency response organization titles, and
- (4) changed the reporting units of Monitor TSW-RIS-5 from counts per minute to Ci per cubic centimeter.
The revisions were compared to their previous revisions, to the criteria of NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, to the criteria of NEI 99-01, "Methodology for Development of Emergency Action Levels," Revision 2, and to the standards in 10 CFR 50.47(b) to determine if the revisions were adequately conducted following the requirements of 10 CFR 50.54(q). This review was not documented in a safety evaluation report and did not constitute approval of licensee changes, therefore, these revisions are subject to future inspection.
The inspector completed two samples during the inspection.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
.1 Barrier Integrity
a. Inspection Scope
The inspectors compared the data from surveillance procedures, operator logs, equipment out-of-service logs, and corrective action logs for the last eleven quarters.
The inspectors verified that Energy Northwest calculated performance indicators in accordance with NEI 99-02, Regulatory Assessment Performance Indicator Guidelines, Revision 4. Performance indicators verified included:
- Reactor Coolant Specific Activity
- Reactor Coolant System Identified Leakage Rate The inspectors completed two samples.
b. Findings
No findings of significance were identified.
.2 Mitigating Systems
a. Inspection Scope
The performance indicators listed below were replaced by the Mitigating Systems Performance Index.
- Heat Removal System
- Emergency AC Power System
- Residual Heat Removal System See Section 4OA5.1 for discussion regarding Temporary Instruction (TI) 2515/169 -
Mitigating Systems Performance Index Verification. This new performance indicator replaced the above mentioned performance indicators which were not required to be verified per Procedure 71151.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Semi-Annual Trend Review
a. Inspection Scope
The inspectors completed an semi-annual trend review of repetitive or closely related issues that were documented in corrective action documents, maintenance records, system health reports, quality assurance audits, and control room logs to identify trends that might indicate the existence of more safety significant issues. The inspectors verified that equipment, human performance, and programmatic issues were being identified by Energy Northwest at an appropriate threshold and were being entered into the corrective action program.
The inspectors completed one sample.
b. Findings and Observations
The inspectors identified an adverse trend associated with degraded flexible electrical conduit jackets resulting in a violation of NRC requirements. See Section 4OA2.5 for more details. No other adverse trends were identified by the inspectors.
.2 Cross-References to PI&R Findings Documented Elsewhere
Section 4OA2.5 describes a finding for the failure to assess corrective action documents in the aggregate resulting in the failure to identify an adverse trend in degraded flexible electrical conduit jackets.
.3 Daily Corrective Action Document Review
a. Inspection Scope
The inspectors performed a review of all documented condition reports and problem evaluation reports to help identify repetitive equipment failures or specific human performance issues for follow-up inspection using other baseline inspection procedures.
The review was accomplished by evaluating Energy Northwests electronic condition report and problem evaluation report databases and attending periodic plant status meetings.
b. Findings
No findings of significance were identified.
.4 Annual Sample - Operator Work Around Review
a. Inspection Scope
On November 29, 2006, the inspectors reviewed the operations department burden list, control room deficiencies, and operator work around list to determine if any operator
work arounds, either individually or collectively, could unnecessarily challenge mitigating system performance or operators during event response. The inspectors verified that Energy Northwest was identifying and documenting operator work around problems at an appropriate threshold.
The inspectors completed one sample.
b. Findings
No findings of significance were identified.
.5 Annual Sample - Adverse Trend in Degraded Electrical Conduit Jackets
a. Inspection Scope
The inspectors reviewed corrective action program records reporting conditions adverse to quality associated with degradation of flexible electrical conduit jackets on various plant electrical components. In some cases, these conduit jackets were credited as a barrier to preclude moisture intrusion into environmentally qualified conduit jackets to support high energy line break calculations. The inspectors reviewed the documents to determine whether operability had been adequately assessed in each case and to ensure that extent of condition had been appropriately considered. Additionally, the inspectors conducted independent walkdowns of various plant components to determine whether degraded conduit jackets existed elsewhere.
The condition reports reviewed by the inspectors included:
- CR 2-05-00341; Flex Conduit Marked 2CMS-4-2 Div-2 Rubber is Split; January 20, 2005
- CR 2-05-03522; Broken Flexible Conduit to Junction Box for MS-V-22D Limit Switches; May 14, 2005
- CR 2-05-04051; MLCS-MO-2A Has Damaged Conduit Which Requires Repair; May 23, 2005
- CR 2-05-04057; MS-V-106A Limit Switch Conduit Damaged; May 23, 2005
- CR 2-05-04328; Panel E-CP-DG/EP3 has severely damaged flexible conduit; May 27, 2005
- CR 2-05-04635; CIA-V-764 has flex conduit pulled loose from the conduit fitting with cables visible; June 3, 2005
- CR 2-05-04636; CIA-V-766 has flex conduit pulled loose from the conduit fitting with cables visible; June 3, 2005
b. Findings
Introduction.
The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for failing to promptly identify conditions adverse to quality associated with loss of full environmental qualification of plant components due to degraded flexible electrical conduit jackets. This finding had a crosscutting aspect associated with problem identification and resolution with a corrective action program causal factor.
Description.
During a walkdown of various plant areas and components, the inspectors identified multiple examples of breeches in flexible conduit hermetic sealing jackets in the Reactor Building. Some of these components were required to be environmentally qualified (i.e., moisture barrier) in the event of a high energy line break. Energy Northwest documented the inspectors observations in the corrective action program as listed below:
- CR 2-06-00142; Low Pressure Core Spray Motor (LPCS-M-P/1) space heater flex has a small hole exposing the inner metal sheath; July 12, 2006
- CR 2-06-05340; The flex conduit jacket for the power supply to RCIC-MO-68 has a slight separation at the connection to the motor operator; July 19, 2006
- CR 2-06-07101; NRC Inspector Identified Conduit Concerns in Reactor Building Pump Rooms; September 26, 2006
- CR 2-06-07293; Issues identified by the NRC resident with the Reactor Building 572 foot level conduits; October 3, 2006
- CR 2-06-07441; NRC Resident Inspector Reported that the Power Supply Cable to MSLC-V-1D Rubber Jacket is torn; October 11, 2006 The inspectors were concerned because degradation of the conduit jacket associated with safety-related components, such as RCIC-MO-68, could result in the component not meeting its environmental qualification requirements.
As a result of the deficiencies documented above during NRC walkdowns and previous deficiencies discovered by Energy Northwest, an adverse trend in the condition of flexible electrical conduit jacket material was documented by Energy Northwest in PER 206-0557, dated October 12, 2006. When degraded flexible electrical conduit jackets were found they were repaired. Further walkdowns by Energy Northwest (as directed by Action Item Number A-247252) and walkdowns by the inspectors identified additional degraded flexible electrical conduit jackets and environmental qualification issues on safety-related components throughout the plant as listed below:
- CR 2-06-07493; Concerns identified by the NRC on 10/12/2006 with flexible conduits and conduit fittings; October 13, 2006
- CR 2-06-07509; Conduit problems identified by NRC during walkdown; October 13, 2006
- CR 2-06-07505; CRD-HCU-3043 has a damaged flexible conduit; October 13, 2006
- CR 2-06-07503; CRD-HCU-1051 has a damaged flexible conduit; October 13, 2006
- CR 2-06-07739; Damaged Flex Conduit on multiple pieces of Plant equipment in the Turbine Building, Feed Pumps, Booster Pumps and Fire Protection Panel; October 15, 2006
- CR 2-06-07735; CMS-RE-12/1B Detector Cable Clamp Needs Repair; October 21, 2006
- CR 2-06-07780; While performing walkdown of the CRD pump room the following issues were identified; October 24, 2006
- CR 2-06-07845; Flexible Conduit issues identified on 471' RB and in DG2 room HVAC panel, 2 issues identified by NRC resident inspector, 1 identified by Energy Northwest; October 25, 2006
- CR 2-06-08015; IRM detector cable IRM-DET-2C found damaged during forced outage FO-06-01; November 2, 2006
- CR 2-06-08087; Degraded Flexible Electrical Conduit Jackets that are split may create additional strainer debris not accounted for in calculation ME-02-97-03; November 3, 2006 NUREG-0588, Interim Staff Position on Environmental Qualification of Safety-Related Electrical Equipment, Revision 1, provides that, Equipment that is used to perform a necessary safety function must be capable of maintaining functional operability under all service conditions postulated to occur during the installed life for the time it is required to operate. The qualification method for this equipment shall establish that each type of equipment is qualified for its application as required by Paragraph 5, Method and Documentation, IEEE 323-1971, General Guide for Qualifying Class I Electric Equipment for Nuclear Power Generating Stations, Revision dated April 1971. Energy Northwest calculation EI-02-86-02, Revision 0, dated April 3, 1986, concludes that the life expectancy of flexible electrical conduit jackets is greater than 40 years under specified temperatures and radiation levels. Energy Northwest determined, as documented in PER 206-0664, dated December 8, 2006, that samples of degraded flexible electrical conduit jackets taken from the Reactor Building and Turbine Building showed that jacket degradation occurs in areas of high stress such as tight bends or buckles in the jacket. Energy Northwest postulated that this most likely would have occurred during initial installation of the conduit. This additional stress was not accounted for in environmental qualification design calculations. As a result, some conduit jacket had degraded and failed prematurely before reaching its expected design environmental qualification lifetime.
After extent of condition walkdowns by engineering staff, flexible electrical conduits jackets for two safe shutdown components were found to be not fully environmentally qualified due to bend radius in the electrical conduits being exceeded as specified per PPM 10.25.57, Electrical Raceway Installation, Revision 29, Attachment 9.1. The affected components were containment instrument air pressure Switch CIA-PS-21A and a containment monitoring system pressure Transmitter CMS-PT-5 limit switch.
CIA-PS-21A pressure switch is part of the actuation logic which supports the automatic depressurization system function. CMS-PT-5 provides post accident monitoring of primary containment pressure. Although the conduit bend radius was exceeded, the conduit jacket had not degraded to the point of it being breached.
Analysis.
The performance deficiency associated with this finding was Energy Northwests failure to promptly identify degraded conduit jackets required to be intact to support full environmental qualification (conditions adverse to quality). This occurred as a result of Energy Northwest failing to identify an adverse trend in conduit jacket material condition although several condition reports written during 2005 and 2006 documented degraded conduit jackets on plant components. The finding was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to preclude undesirable consequences (i.e., core damage). The finding was determined to be of very low safety significance because, although the qualification for high energy line break was affected for some components, the finding did not result in inoperability of any equipment. Additionally, the finding was a qualification deficiency confirmed not to result in loss of operability per Part 9900 Technical Guidance, Operability Determination Process for Operability and Functional Assessment. This finding had a crosscutting aspect associated with problem identification and resolution with a corrective action program casual factor. Specifically, Energy Northwest failed to assess and trend information from the corrective action program in the aggregate resulting in the failure to identify an adverse trend regarding flexible electrical conduit jackets.
Enforcement.
10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires in part that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances are promptly identified and corrected. Full qualification requires that environmental barriers (moisture seals) be effective during a predetermined qualified life as required by NUREG-0588 and IEEE 323-1971. Contrary to this requirement, prior to October 12, 2006, the station failed to take action to promptly identify degraded flexible electrical conduit jackets, conditions adverse to quality. Consequently, a violation of 10 CFR Part 50, Appendix B, Criterion XVI, was identified by the inspectors. Because this finding was of very low safety significance and was entered into the licensees corrective action program as PER 206-0557, this violation is being treated as an NCV, consistent with Section VI.A.1 of the Enforcement Policy (NCV 0500097/2006005-03; Failure to Promptly Identify Degraded Conduit Jacket). Energy Northwest plans to further assess the operability of safe shutdown equipment by:
- (1) ensuring that Rosemount transmitter MS-PT-51B is sealed with Dow Corning foam. This is will ensure that this transmitter has a qualified moisture barrier and would restore the component to full qualification.
- (2) Complete walkdowns of high energy line break affected areas for flexible conduit condition and repair flexible conduit
damage if evident.
- (3) Revise Drawing M937 to require annual inspections of safe shutdown equipment conduit jackets and tape repairs for integrity. Full qualification will be achieved when the first inspection (see item number 2 above) is completed and the drawing is updated to reflect that annual inspections are required.
4OA3 Event Follow-up
.1 Automatic Scram on October 31, 2006
a. Inspection Scope
On October 31, 2006, the inspectors observed and evaluated Energy Northwests response to an automatic reactor scram from 100 percent power. The scram initiated when the high pressure turbine throttle valves and governor valves closed as a result of a digital electrical hydraulic system circuit card failure. Per design, an automatic reactor scram occurred when the throttle valves were less than 95 percent open. The inspectors responded to the control room and verified the status of plant conditions by observing key plant parameters, annunciator status, and observing the current status of safety-related mitigating equipment to ensure that the reactor plant was stable. The inspectors also observed reactor operator actions in response to the reactor scram and senior reactor operators evaluation of plant conditions and oversight of the reactor operators to ensure that operators were adhering to plant procedures.
b. Findings
No findings of significance were identified
.2 Reactor Level and Reactor Power Transient During Startup on November 7, 2006
a. Inspection Scope
On November 7, 2006, the inspectors observed and evaluated Energy Northwests response to a reactor level and reactor power transient during startup. While raising reactor pressure from 600 psig to 935 psig via the digital electrical hydraulic system in auto, a reactor pressure vessel level and reactor power transient occurred. As reactor pressure vessel pressure increased, the discharge pressure of the operating reactor feed water pump was not raised sufficiently to ensure continued feeding of the reactor pressure vessel. As a consequence, reactor feedwater flow reduced resulting in lowering vessel level. Control room staff noted a slowly lowering trend in vessel level and increased reactor feedwater pump speed and discharge pressure to increase feedwater flow to the reactor vessel. Vessel level was noted to lower to 33 inches. The increase in feedwater flow resulted in the addition of relatively colder feedwater resulting in a slight power increase, receipt of an average power range monitor high rod block alarm, and vessel level peaking at 43 inches. Operators subsequently returned reactor pressure vessel water level to normal. Energy Northwest subsequently concluded that inadequate control room supervisory oversight resulted in the failure of the reactor operator to receive information regarding the command to raise vessel pressure using the main turbine control system. The inspectors performed an independent assessment of the circumstances of the event and did not identify any significant issues.
Additionally, the inspectors verified that fuel thermal limits were not exceeded during the event.
b. Findings
No findings of significance were identified.
.3 (Closed) LER 05000397/2005-005 - Inoperable Standby Liquid Control Pump Due to
Incorrect Fuse On July 28, 2005, Energy Northwest identified that an incorrect fuse had been installed in the circuitry associated with standby liquid control pump 1A. The incorrect fuse was installed during a maintenance activity on July 6, 2005, and resulted in the pump being inoperable for approximately 22 days. Energy Northwest replaced the fuse with the correct type and declared the pump operable. See IR 05000397/2005-004, Section 4OA7.2, for discussion of an associated licensee identified NCV. The inspectors did not identify any other significant findings or violations of NRC requirements during their review of the LER. Energy Northwest documented the issue in PER 205-0502.
4OA5 Other Activities
.1 Temporary Instruction (TI) 2515/169 - Mitigating Systems Performance Index
Verification
a. Inspection Scope
On November 30, 2006, the inspectors completed an inspection in accordance with Temporary Instruction 2515/169, Mitigating Systems Performance Index Verification, to verify that the licensee correctly implemented the Mitigating System Performance Index (MSPI) guidance.
The inspectors reviewed the data the licensee used to generate the basis document unavailability and unreliability values. The licensee entered the values into a spreadsheet which was used to perform various calculations. The inspectors also used the following licensee source documents to verify the validity of the input data:
- Control Room Logs
- Surveillance Test Procedures
- Maintenance Procedures
b. Findings
No findings of significance were identified. The inspectors concluded that the licensee is monitoring, collecting and entering the appropriate data in accordance to the prescribed guidance.
Per the temporary instruction, the inspectors assessed and answered the following questions:
Question Answer For the sample selected, did the licensee accurately document the baseline Yes planned unavailability hours for the MSPI systems?
For the sample selected, did the licensee accurately document the actual Yes unavailability hours for the MSPI systems?
For the sample selected, did the licensee accurately document the actual Yes unreliability information for each MSPI monitored component?
Did the inspector identify significant errors in the reported data, which No resulted in a change to the indicated index color?
Did the inspector identify significant discrepancies in the basis document which resulted in
- (1) a change to the system boundary;
- (2) an addition of a No monitored component; or
- (3) a change in the reported index color?
.2 (Closed) URI 05000397/2006004-01: Non-Venting of Alternate Boron Injection Hose
Introduction.
An NRC identified Green NCV of TS 5.4.1.a was identified for the failure to provide an adequate procedure for alternate boron injection. Specifically, procedure Emergency Support Procedure (ESP) 5.5.8, Alternate Boron Injection, Revision 8, failed to direct venting of a temporarily installed hose between the standby liquid control boron storage tank and the reactor core isolation cooling (RCIC) Pump RCIC-P-1 suction. As a result, air introduction into RCIC-P-1 upon initiation of alternate boron injection during low flow operations could adversely affect RCIC-P-1 performance.
Description.
As documented in IR 0500397/2006004, Section 1R04.2, the inspectors identified that procedure ESP 5.5.8 did not direct venting of a temporarily installed hose between the outlet of the standby liquid control boron storage tank (approximate 548 foot elevation) and the suction of the reactor core isolation cooling pump (approximate 422 foot elevation). This hose connection allowed the contents of the boron storage tank to be injected into the reactor coolant system via RCIC-P-1 to provide for a diverse method of shutting down the reactor in the event that AC power was not available to operate the standby liquid control pumps in response to an anticipatory transient without scram event. The inspectors were concerned that by not venting the hose that air (approximately 4.3 cubic feet) could be inadvertently injected into the suction of RCIC-P-1 causing the pump to lose net positive suction head and adversely impact pump performance. URI 05000397/2006004-01 was opened pending the NRCs review of Energy Northwests evaluation of the adequacy of not venting the temporarily installed hose prior to initiating alternate boron injection via RCIC-P-1.
Energy Northwest documented the concern in CR 2-06-06510.
The inspectors reviewed Energy Northwests evaluation of CR 2-06-06510 and an associated evaluation (PTLA 252435) and noted that Energy Northwest concluded that RCIC-P-1 would not become airbound due to the following:
- With the RCIC system operating at 600 gpm (rated flow), that RCIC-P-1 would not become air bound during alternate boron injection without venting.
- At less than 350 gpm RCIC-P-1 pump flow, RCIC-P-1 could potentially meet or exceed 8 percent air entrainment by volume during alternate boron injection without venting. Air entrapment greater than 8 percent has the potential to cause air binding. However, due to the short duration that the pump could have been exposed to greater than 8 percent air by volume, the pump vendor does not anticipate that air in the temporarily installed hose would present a problem for RCIC-P-1.
- The probability that RCIC-P-1 would be operated at less than 350 gpm at the time it would be needed for alternate injection of boron is very low. RCIC-P-1 typically runs in automatic at 600 gpm. Additionally, operators would be expected to operate RCIC-P-1 at rated flow of 600 gpm in the event that RCIC-P-1 is needed for boron injection to maximize the rate of boron injection.
Additionally, while RCIC-P-1 can be taken to manual control to achieve flow rates less than 600 gpm, operations procedures contain notes cautioning against operating RCIC-P-1 at flow rates less than 300 gpm.
However, Energy Northwest also determined that per PPM 5.1.2, RPV Control -
ATWS, Revision 17, it is possible for an operator to maintain RPV level using RCIC while concurrently using RCIC to add boron via Procedure ESP 5.5.8. Therefore, RCIC flow could be throttled to maintain RPV level at a flow rate less than 350 gpm. If boron injection occurred per Procedure ESP 5.5.8 with RCIC-P-1 operating at less than 350 gpm, it would be possible for RCIC-P-1 to experience decreased performance due to the air-water volume exceeding 8 percent.
Although it was unlikely that RCIC-P-1 would become air bound as a result of not venting the installed hose prior to initiating alternate boron injection, the inspectors noted that Energy Northwests evaluation concluded that RCIC-P-1 performance could be adversely affected during low flow conditions (300 - 350 gpm) where the percent air by volume would exceed 8 percent. As a result, the inspectors concluded that procedure ESP 5.5.8 was not adequate in that acceptable RCIC-P-1 performance was not assured without venting the temporarily installed hose prior to initiating alternate boron injection. The inspectors noted that Energy Northwest revised procedure ESP 5.5.8 on October 27, 2006, to direct venting the temporarily installed hose prior to initiation of alternate boron injection.
Analysis.
The performance deficiency associated with this finding is Energy Northwests failure to ensure that Procedure ESP 5.5.8 was adequate in accordance with TS 5.4.1.a.
Specifically, Procedure ESP 5.5.8 failed to direct venting of a temporarily installed hose between the outlet of the standby liquid control boron storage tank and suction of RCIC-P-1. As a result, air introduction into the suction of RCIC-P-1 upon initiation of alternate boron injection, during conditions of low flow operation of RCIC-P-1, could result in decreased performance of RCIC-P-1. This NRC identified finding was more than minor because the finding had an attribute of procedure quality which affected the mitigating systems cornerstone objective to ensure the availability and reliability of systems that respond to initiating events to prevent undesirable consequences. Utilizing
MC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations, Phase 1 screening, the inspectors determined that the finding was of very low risk significance (Green) because, although degraded reactor core insolation cooling pump performance could occur, the pump was expected to perform adequately to support alternate boron injection, based on Energy Northwests engineering evaluation. Additionally, the finding was not a qualification issue confirmed not to result in loss of operability, did not represent a loss of safety function for a single train or for the system, and did not screen as potentially risk significant due to external events.
Enforcement.
Technical Specification 5.4.1.a, requires in part that written procedures shall be established and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Quality Assurance Program Requirements (Operation), Revision 2, Appendix A, Section 6.n, provides in part that emergency procedures be established for conditions requiring use of emergency boration or standby liquid control system.
Contrary to this requirement, since August 23, 1990, Procedure ESP 5.5.8 was inadequate in that it did not provide for venting of a temporarily installed hose between the boron storage tank and the suction of RCIC-P-1. As a result, RCIC-P-1 could experience decreased performance during operations below 350 gpm. Because this finding was of very low safety significance and was entered into the licensees corrective action program as CR 2-06-06510, this violation is being treated as an NCV, consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000397/2006005-04, Inadequate Alternate Boron Injection Procedure). Energy Northwest revised procedure ESP 5.5.8 to vent the temporarily installed hose.
4OA6 Meetings, Including Exit
On November 6, 2006, the inspector presented the emergency plan change inspection results to Mr. M. Reis, Supervisor, Emergency Preparedness. The inspector confirmed that proprietary information was not provided or examined during the inspection.
On November 16, 2006, the inspectors presented the safety evaluation and permanent plant modifications inspection results to Mr. S. Oxenford, Vice President of Technical Services, and other members of the staff who acknowledged those results. No proprietary information was included in this report.
On December 14, 2006 the inspector debriefed the inspection results with Mr. Louis Cortopassi, Training Manager, and other members of the licensees staff at the conclusion of the inspection. A telephone exit was held with Mr. Michael Cantrell on January 10, 2007. The licensee acknowledged the findings presented in both the briefing and the final exit meeting. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
On January 11, 2007, the resident inspectors presented the inspection results to Mr. Atkinson and other members of his staff who acknowledged the findings. The inspectors confirmed that proprietary information was not provided or examined during the inspection.
4OA7 Licensee Identified Violations
None.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Energy Northwest
- D. Atkinson, Vice President, Nuclear Generation
- S. Belcher, Manager, Operations
- I. Borland, Manager, Radiation Protection
- S. Boynton, Manager, Systems Engineering
- M. Cantrell, Manager, Operations Training
- D. Coleman, Manager, Performance Assessment and Regulatory Programs
- L. Cortopassi, Manager, Training
- G. Cullen, Licensing Supervisor, Regulatory Programs
- J. Dittmer, Supervisor, Design Engineering
- M. Eades, Licensing Engineer, Regulatory Programs
- D. Gregoire, Supervisor Licensing (Acting), Regulatory Programs
- R. Jorgenson, Senior Emergency Planner
- A. Khanpour, General Manager, Engineering
- T. Lynch, Plant General Manager
- S. Mazurkiewicz, Licensing Engineer
- T. North, Supervisor, Operator Training, Requalification
- W. Oxenford, Vice President, Technical Services
- J. Parrish, Chief Executive Officer
- J. Redwine, Simulator Supervisor
- M. Reis, Supervisor, Emergency Preparedness
- N. Richmond, Senior Occupational Health/Nurse
- F. Schill, Licensing
- R. Torres, Manager, Quality Assurance
- C. Whitcomb, Vice President, Organizational Performance and Staffing
NRC Personnel
- J. Bashore, Project Engineer
- F. Brush, Senior Project Engineer
- R. Cohen, Resident Inspector and Temporary Senior Resident Inspector
- Z. Dunham, Senior Resident Inspector
ITEMS OPENED AND CLOSED
Items Opened, Closed, and Discussed During this Inspection
Opened
05000397/2006005-01 URI Loss of Shutdown Cooling (Section 1R20)
Attachment
Opened and Closed
05000397/2006005-02 NCV Failure to Follow Diesel Generator Surveillance Test
Procedure (Section 1R22)05000397/2006005-03 NCV Failure to Promptly Identify Degraded Conduit Jacket
(4OA2.5)05000397/2006005-04 NCV Inadequate Alternate Boron Injection Procedure (Section
4OA5.2)
Closed
05000397/2005-005-00 LER Inoperable Standby Liquid Control Pump Due to Incorrect
Fuse (Section 4OA3.2)05000397/2006004-01 URI Non-Venting of Alternate Boron Injection Hose (Section
4OA5.2)
Discussed
None.
PARTIAL