IR 05000317/2013008

From kanterella
Revision as of 13:03, 18 May 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
IR 05000317-13-008 and 05000318-13-008; 09/09/2013 - 09/27/2013; Calvert Cliffs Nuclear Power Plant, Units 1 and 2 (Ccnpp); Biennial Baseline Inspection of Problem Identification and Resolution
ML13310A554
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 11/05/2013
From: Schroeder D L
Reactor Projects Branch 1
To: Gellrich G H
Constellation Energy Nuclear Group
Schroeder D L
References
IR-13-008
Download: ML13310A554 (16)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 2100 RENAISSANCE BOULEVARD, SUITE 100 KING OF PRUSSIA, PENNSYLVANIA 19406-2713 November 5, 2013 Mr. George H. Gellrich, Vice President Calvert Cliffs Nuclear Power Plant Constellation Energy Nuclear Group, LLC

1650 Calvert Cliffs Parkway Lusby, MD 20657-4702

SUBJECT: CALVERT CLIFFS NUCLEAR POWER PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT

05000317/2013008 AND 05000318/2013008

Dear Mr. Gellrich:

On September 27, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Calvert Cliffs Nuclear Power Plant, Units 1 and 2. The enclosed report documents the inspection results, which were discussed on September 27, 2013, with you and other members of your staff.

This inspection examined activities conducted under your license as they relate to identification and resolution of problems and compliance with the Commission's rules and regulations and conditions of your license. Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel.

Based on the samples selected for review, the inspectors concluded that Constellation was generally effective in identifying, evaluating, and resolving problems. Constellation personnel identified problems and entered them into the corrective action program (CAP) at a low threshold. Constellation prioritized and evaluated issues commensurate with the safety significance of the problems and corrective actions were generally implemented in a timely manner.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Managem ent System (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA RPowell for/

Daniel L. Schroeder, Chief Reactor Projects Branch 1

Division of Reactor Projects

Docket Nos: 50-317 and 50-318 License Nos: DPR-53 and DPR-69

Enclosure: Inspection Report 05000317/2013008 and 05000318/2013008 w/Attachment: Supplemental Information cc w/encl: Distribution via ListServ

ML13310A554 SUNSI Review Non-Sensitive Sensitive Publicly Available Non-Publicly Available OFFICE RI/DRP RI/DRP RI/DRP NAME SBarber/SB RPowell/RP DSchroeder/RP for DATE 11/1/13 11/5/13 11/5/13

Enclosure 1 U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos: 50-317 and 50-318

License Nos: DPR-53 and DPR-69

Report No: 05000317/2013008 and 05000318/2013008

Licensee: Constellation Energy Nuclear Group, LLC (Constellation)

Facility: Calvert Cliffs Nuclear Power Plant, Units 1 and 2 (CCNPP)

Location: Lusby, MD

Dates: September 9 - 13, 2013 September 23 - 27, 2013

Team Leader: S. Barber, Senior Project Engineer, Division of Reactor Projects (DRP)

Inspectors: H. Gray, Senior Reactor Inspector, Division of Reactor Safety E. Torres, Resident Inspector, DRP S. McCarver, Reactor Inspector, DRP

Approved by: Daniel L. Schroeder, Chief Reactor Projects Branch 1 Division of Reactor Projects

Enclosure 2

SUMMARY OF FINDINGS

IR 05000317/2013008 and 05000318/2013008; 09/09/2013 - 09/27/2013; Calvert Cliffs Nuclear

Power Plant, Units 1 and 2 (CCNPP); Biennial Baseline Inspection of Problem Identification and Resolution.

This NRC team inspection was performed by one resident inspector and three regional inspectors. No findings were identified during this inspection. The NRC' s program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

Problem Identification and Resolution

The inspectors concluded that Constellation was generally effective in identifying, evaluating, and resolving problems. Constellation personnel identified problems, entered them into the CAP at a low threshold, and prioritized issues commensurate with their safety significance. In most cases, Constellation appropriately screened issues for operability and reportability, and performed causal analyses that appropriately considered extent of condition, generic issues, and previous occurrences. The inspectors also determined that Constellation typically implemented corrective actions to address the problems identified in the CAP in a timely manner. The inspectors concluded that, in general, Constellation adequately identified, reviewed, and applied relevant industry operating experience to Calvert Cliffs operations. In addition, based on those items selected for review, the inspectors determined that Constellation self-assessments and audits were thorough.

Based on the interviews the inspectors conducted over the course of the inspection, observations of plant activities, and reviews of individual CAP and employee concerns program issues, the inspectors did not identify any indications that site personnel were unwilling to raise safety issues nor did they identify any conditions that could have had a negative impact on the site's safety conscious work environment.

3

REPORT DETAILS

OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution

This inspection constitutes one biennial sample of problem identification and resolution as defined by Inspection Procedure 71152. All documents reviewed during this inspection are listed in the Attachment to this report.

.1 Assessment of Corrective Action Program Effectiveness

a. Inspection Scope

The inspectors reviewed the procedures that described Constellation Energy Nuclear Group, LLC's (CENG) corrective action program (CAP) at Calvert Cliffs. To assess the effectiveness of the CAP, the inspectors reviewed performance in three primary areas:

problem identification, prioritization and evaluation of issues, and corrective action implementation. The inspectors compared performance in these areas to the requirements and standards contained in 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," and CNG-CA-1.01-1000, "Corrective Action Program." For each of these areas, the inspectors considered risk insights from the station's risk analysis and reviewed condition reports selected across the seven cornerstones of safety in the NRCs Reactor Oversight Process. Additionally, the inspectors attended multiple Plan-of-the-Day, Condition Report Screening, and Management Review Committee meetings. The inspectors selected items from the following functional areas for review: engineering, operations, maintenance, emergency preparedness, radiation protection, chemistry, physical security, and oversight programs.

(1) Effectiveness of Problem Identification

In addition to the items described above, the inspectors reviewed system health reports, a sample of completed corrective and preventative maintenance work orders, completed surveillance test procedures, operator logs, and periodic trend reports. The inspectors also completed field walkdowns of various systems on site, such as the emergency diesel generators, station battery 11, 12, 21 and 22 rooms, component cooling head tanks, component cooling pump rooms, service water head tanks, refueling water tanks to ensure that observable deficiencies were documented.

Additionally, the inspectors reviewed a sample of condition reports (CRs) written to document issues identified through internal self-assessments, audits, emergency preparedness drills, and the operating experience program. The inspectors completed this review to verify that Constellation entered conditions adverse to quality into their CAP as appropriate.

(2) Effectiveness of Prioritization and Evaluation of Issues

The inspectors reviewed the evaluation and prioritization of a sample of CRs issued since the last NRC biennial Problem Identification and Resolution inspection completed in September 2011. The inspectors also reviewed CRs that were assigned lower levels of significance that did not include formal cause evaluations to ensure that they were properly classified. The inspectors' review included the appropriateness of the assigned significance, the scope and depth of the causal analysis, and the timeliness of 4 resolution. The inspectors assessed whether the evaluations identified likely causes for the issues and developed appropriate corrective actions to address the identified causes. Further, the inspectors reviewed equipment operability determinations, reportability assessments, and extent-of-condition reviews for selected problems to verify these processes adequately addressed equipment operability, reporting of issues to the NRC, and the extent of the issues.

(3) Effectiveness of Corrective Actions The inspectors reviewed Constellation's completed corrective actions through documentation review and, in some cases, field walkdowns to determine whether the actions addressed the identified causes of the problems. The inspectors also reviewed CRs for adverse trends and repetitive problems to determine whether corrective actions were effective in addressing the broader issues. The inspectors reviewed Constellation's timeliness in implementing corrective actions and effectiveness in precluding recurrence for significant conditions adverse to quality. The inspectors also reviewed a sample of CRs associated with selected non-cited violations (NCVs) and findings to verify that Constellation's personnel properly evaluated and resolved these issues. The inspectors also reviewed a sample of CRs associated with selected NCVs, findings, and licensee event reports to verify that Constellation personnel properly evaluated and resolved these issues. In addition, the corrective action review was expanded to five years to evaluate Constellation's actions related to system performance issues identified for the 125 VDC system.

b. Assessment

(1) Effectiveness of Problem Identification Based on the samples selected, the inspectors determined that, in general, Constellation identified problems and entered them into the CAP at a low threshold. Constellation personnel at Calvert Cliffs initiated approximately 23,000 CRs between September 2011 and September 2013. Based on the samples reviewed, the inspectors determined that Constellation trended equipment and programmatic issues, and appropriately identified problems in CRs. The inspectors verified that conditions adverse to quality identified through this review were entered into the CAP as appropriate. Additionally, inspectors concluded that personnel were identifying trends at low levels. In general, inspectors did not identify any issues or concerns that had not been appropriately entered into the CAP for evaluation and resolution. In response to several questions and minor equipment observations identified by the inspectors during plant walkdowns, Constellation personnel promptly initiated CRs and/or took immediate action to address the issues.

5

(2) Effectiveness of Prioritization and Evaluation of Issues The inspectors determined, based on the samples selected, that Constellation, in general, appropriately prioritized and evaluated issues commensurate with the safety significance of the identified problem. CRs were screened for operability and reportability, categorized by significance, and assigned to a department for evaluation and resolution. The inspectors observed the various CR screening and management review groups and noted that they considered equipment operability and reportability, human performance issues, radiological safety concerns, repetitiveness, adverse trends, and potential impact on safety conscious work environment (SCWE) during the conduct

of these reviews.

Items reviewed by the inspectors during the inspection were categorized for evaluation and resolution commensurate with the significance of the issues. Guidance provided by Constellation procedure, CNG-CA-1.01-1000, "Corrective Action Program," for categorization appeared sufficient to ensure consistent implementation based on the sample of CRs reviewed by the inspectors. In general, issues were appropriately screened and prioritized commensurate with their safety significance.

The inspectors reviewed a sample of root cause analyses with included common cause analyses, apparent cause analyses, and a number of individual CR evaluations. For the evaluations reviewed, the inspectors noted that Constellation's evaluations were generally thorough and appropriately considered extent of condition, generic issues, and previous occurrences.

(3) Effectiveness of Corrective Actions The inspectors concluded that corrective actions for identified deficiencies were typically timely and adequately implemented. The inspectors also concluded that Constellation performed in-depth effectiveness reviews for significant issues to verify that implemented corrective actions were effective. The inspectors' review of the CR disposition documentation and verification of corrective action implementation showed that Constellation routinely developed adequate corrective action as evidenced by the lack of repetitive events. The inspectors also reviewed corrective actions for the 125 VDC

system for the last five years to evaluat e Constellation's actions for various system performance issues and noted comprehensive actions for significant issues, and reasonable corrective actions for minor issues.

c. Findings

No findings were identified.

.2 Assessment of the Use of Operating Experience (OE)

a. Inspection Scope

The inspectors reviewed a sample of CRs associated with review of industry OE to determine whether Constellation appropriately evaluated the OE information for applicability to Calvert Cliffs and had taken appropriate actions, when warranted. The inspectors also reviewed evaluations of OE documents associated with a sample of NRC generic communications to ensure that Constellation adequately considered the 6 underlying problems associated with the issues for resolution via their CAP. In addition, the inspectors observed various plant activities to determine if the station considered industry OE during the performance of routine and infrequently performed activities.

b. Assessment The inspectors determined that Constellation appropriately considered industry OE

information for applicability, and used the information for corrective and preventive actions to identify and prevent similar issues when appropriate. The inspectors determined that OE was appropriately applied and lessons learned were communicated and incorporated into plant operations and procedures when applicable. The inspectors also observed that industry OE was routinely discussed and considered during the conduct of condition report screening meetings and pre-job briefs.

c. Findings

No findings were identified.

.3 Assessment of Self-Assessments and Audits

a. Inspection Scope

The inspectors reviewed a sample of audits, including the most recent audit of the CAP, departmental self-assessments, and assessments performed by independent organizations. These reviews were performed to determine if problems identified through these assessments were entered into the CAP when appropriate and whether corrective actions were initiated to address identified deficiencies. The effectiveness of the audits and assessments was evaluated by comparing audit and assessment results against self-revealing and NRC-identified observations made during the inspection.

b. Assessment The inspectors concluded that self-assessments, audits, and other internal Constellation assessments were generally critical, probing, thorough, and effective in identifying issues. The inspectors observed that these audits and self-assessments were completed in a methodical manner by personnel knowledgeable in the subject matter. The audits and self-assessments were completed to a sufficient depth to identify issues that were entered into the CAP for evaluation. In general, corrective actions associated with the identified issues were implemented commensurate with their safety significance.

c. Findings

No findings were identified.

4. Assessment of Safety Conscious Work Environment

a. Inspection Scope

During interviews with station personnel, the inspectors assessed the safety conscious work environment at Calvert Cliffs. Specifically, the inspectors interviewed personnel to determine whether they were hesitant to raise safety concerns to their management 7 and/or the NRC. The inspectors also interviewed the station Employee Concerns Program coordinator to determine what actions are implemented to ensure employees were aware of the program and its availability with regards to raising safety concerns. The inspectors reviewed the Employee Concerns Program files to ensure that Constellation entered issues into the CAP, when appropriate.

b. Assessment During interviews, Calvert Cliffs staff expressed a willingness to use the CAP to identify plant issues and deficiencies and stated that they were willing to raise safety issues. The inspectors noted that no one interviewed stated that they personally experienced or were aware of a situation in which an individual had been retaliated against for raising a safety issue. All persons interviewed demonstrated an adequate knowledge of the CAP and the Employee Concerns Program. Based on these limited interviews, the inspectors concluded that there was no evidence of an unacceptable safety conscious work environment and no significant challenges to the free flow of information.

c. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On September 27, 2013, the inspectors presented the inspection results to Mr. George Gellrich, Site Vice President, and other members of the Calvert Cliffs staff. The inspectors confirmed that proprietary information was reviewed by inspectors during the course of the inspection, that any proprietary information that was reviewed was returned to Constellation, and that the content of this report includes no proprietary information.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

G. Gellrich, Site Vice President
M. Flaherty, Plant General Manager
S. Henry, Manager, Operations
D. Lauver, Director, Licensing
D. Dellario, Manager, Engineering
H. Daman, Manager, Maintenance
M. Jones, Director, Performance Improvement Unit
C. Neyman, Senior Engineering Analyst, Licensing
J. Schoolcraft, Performance Improvement Unit
J. Phifer, Senior Analyst, Quality and Performance Assessment
S. Loeper, Principal Engineer, System Engineering
E. Kreahling, Principal Engineer, System Engineering
R. Jones, Supervisor, Engineering Programs
C. Grooms, General Supervisor, Operations Support
L. Smith, General Supervisor, Engineering Asset Management
G. Dare, Senior Engineering Analyst, System Engineering
M. Major, Senior Engineering Analyst, System Engineering
R. Bleacher, Operations Technical Writer
J. Gaines, General Supervisor Shift Operations
P. Beavers, General Supervisor Operations Training
R. Stark, Design Engineer
J. Wynn, System Engineer
C. Conover, Chemistry Supervisor
J. Stone, Supervisor Engineering

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

None

LIST OF DOCUMENTS REVIEWED

Section 4OA2: Identification and Resolution of Problems

Audits and Self-Assessments
SEC-12-01-C, Security, Access Authorization & Fitness For Duty Programs
SEC-13-01-C, Access Authorization & Fitness For Duty Programs
OPS-12-01-C, Nuclear Operations Program
SA-2012-000003, OE Program Focused Self-Assessment
SA-2012-000005, Department Corrective Action Review Team (DCART) Effectiveness Self-Assessment Attachment
SA-2013-000119, EPRI guidelines for diesel generator Sulfate, feed and bleed strategies
MAI-13-01-C, Maintenance Program Audit
CHE-13-01-C, Chemistry Program
BM-2012-00032, Benchmark on Emergency Preparedness, post Seismic
BM-2011-00225, Benchmark on Water Treatment to reduce corrosion
BM-2013-00119, Benchmark on Closed Cooling Water chemistry

Condition Reports

(CRs)

  • 2013-007311
  • 2013-007318
  • 2013-007337
  • 2013-007377
  • 2013-007379
  • 2013-007626
2008-001434
2009-004927
2010-009891 2010-010103
2010-010486
2010-011675
2011-003061
2011-003714 2011-004110
2011-005150
2011-005197
2011-005536
2011-005604 2011-006211
2011-006679
2011-006836
2011-006838
2011-008317
2011-009223 2011-009544
2011-010259
2011-010294
2011-010518
2011-010612
2011-011302
2011-011345
2011-011569
2012-000894
2012-000895
2012-001027
2012-001140 2012-001294
2012-002079
2012-002344
2012-004150
2012-004225 2012-004279
2012-004280
2012-004281
2012-004282
2012-004370
2012-004552
2012-004578
2012-004615
2012-004936
2012-004971
2012-005108
2012-005425
2012-005686
2012-005789
2012-005791 2012-005793
2012-005794
2012-005795
2012-005796
2012-005797
2012-005798
2012-006059
2012-006199
2012-006574
2012-006926
2012-007079
2012-007098
2012-007099
2012-007427
2012-007570
2012-009031
2012-009077 2012-009564
2012-009838
2012-009976
2012-009977
2012-010499
2012-010578 2012-010579
2012-010581
2012-010581
2012-010583 2012-010584
2012-011499
2013-000481 2013-000752
2013-001208
2013-001909
2013-003275
2013-003346
2013-003825
2013-003857
2013-004073 2013-004141
2013-004322
2013-004554
2013-004967
2013-005357
2013-005410
2013-005427
2013-005598
2013-005657
2013-005740
2013-005853
2013-006072
2013-006074
2013-006130
2013-006142
2013-006244
2013-006274
2013-006276
2013-006283
2013-006334
2013-006371
2013-006732
2013-006995
2013-007069
2013-007091
2013-007123
2013-007233
2013-007239
2013-007254
2013-007256
2013-007263
2013-007271
2013-007275
2013-007276
Attachment
2013-007281
2013-007282
2013-007283
2013-007284
2013-007286
2013-007288
  • Identified during this inspection
Non-Cited Violations and Findings 05000317/318/2011005-01, CCNPP Did Not Adequately Prescribe and Implement Procedures Associated with Protected Equipment 05000318/2012004-02, Corrective Actions Not Completed for Drains in the Intake Structure
05000317/318/2013003-02, Inadequate Steam Generator Tube Rupture Emergency Operating

Procedure

05000317/318/2011004-01,Inadequate corrective actions associated with submerged saltwaterpump motor cables 05000317/318/2012002-01, Failure to establish test program for auxiliary feedwater emergency air accumulators 05000317/318/2012009-01, Failure to establish testing program for engineering safety actuation system shutdown sequencer 0500318/2013002-01, Failure to establish adequate design control measures for diesel fuel oil cloud point 05000317/318/2013003-01, Failure to establish a test program for diesel fuel oil check valves
05000317/318/2012003-01, PORV Maintenance Procedure Inadequacy
05000317/318/2011004-01, Inadequate Protected Equipment Controls

Operating Experience

RIS 12-03, Reintegration of Security into the ROP
IN-12-04, Impacts on Normal Plant Operations Due to Leaks or Spills of Chemicals
RIS 12-09, Endorsement of Nuclear Energy Institute Guidance Using an Alternative Method to Manage Cumulative Fatigue at Nuclear Power Reactor Sites
IN 2012-01, Seismic considerations-principally issues involving tanks
IN 2012-03, Design vulnerability in electrical power systems
BM-2013-00107, Benchmark on Steam Generator Management
BM-2011-00193 Benchmark and Self-Assessment on

Operating Experience

(OE) of PI&R related to plant deficiencies

Procedures

CNG-CA-1.01-1000, "Corrective Action Program," Rev. 00902
CNG-CA-1.01-1001, "Management Review Committee," Rev. 00500
CNG-CA-1.01-1003, "Performance Improvement Coordinators," Rev. 00100
CNG-CA-1.01-1004, "Root Cause Analysis," Rev. 00804
CNG-CA-1.01-1005, "Apparent Cause Evaluation," Rev. 00200
CNG-CA-1.01-1007, "Performance Improvement Program Trending and Analysis," Rev. 00200
CNG-CA-1.01-1010, "Use of Operating Experience," Rev. 01000
CNG-CA-1.01-1011, "Management Observation Program," Rev. 00501
CNG-OP-1.01-2010, Operator Workaround/Challenge Control, Revision 00000
CNG-CA-1.01-GL200, "Causal Analysis Handbook," Rev. 00501
CNG-CA-1.01-GL400, "Fleet Trend Codes," Rev. 00600
CNG-CA-1.01-GL700, "Departmental Corrective Action Review Team," Rev. 00100
CNG-CA-1.01-GL800, "Corrective Action Completion Evaluation," Rev. 00200
CNG-CA-2.01-1000, Self-Assessment and Benchmarking Process, Revision 00702
NO-1-123, Managing Operator Impacts, Revision 00101
Attachment
NO-1-200, Control of Shift Activities, Revision 05200
SS-100, Conduct of Security Equipment Modification, Revision 10
CP-0222, Specifications and Surveillance Diesel Generator Jacket Cooling System, Revision
01300
EOP-5, Loos of Coolant Accident, Revision 22
EOP-2, Loos of Offsite Power/Loss of Forced Circulation, Revision 14
EOP-8, Functional Recovery Procedure, Revision 33
AOP-7J, Loss of 120 Volt Vital AC or 125 Volt Vital DC Power, Revision 19
OI-26B, 120 Volt Vital AC and Computer AC, Revision 22
CNG-NL-1.01-1008, "Preparation and Management of External Inspections," Rev 00700
CNG-AM-1.01-1023, Maintenance Rule Program, Rev 00201
CNG-NL-1.01-1008, Preparation and Management of External Inspections, Revision 00700
CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201
MAI-13-01-C, Maintenance Program Audit, Revision 0

Work Orders

C90624813
C91702359
C91851962
C91869686
C91938041
C92092763
C92172212
C92201042
C92234558
C92234559
C92299069
C92311279
C92328793
C92371110
C92405589 Drawings 60727sh0002, Diesel Generator Cooling Water, Starting Air, Fuel, & Lube Oil Diesel No. 1B, Revision 39 60710sh0001, Component Cooling System, Revision 39 63017sh0002, Single Line Diagram Reactor 480V
MCC 214R, Revision 44 63017sh0001, Single Line Diagram Reator 480V
MCC 204R, Revision 44 61017sh0001, Single line Diagram Reactor 480V
MCC 104R, Revision 41 61017sh0002, Single line Diagram Reactor 480V
MCC 114R, Revision 45
63022, Single Line Diagram 120V AC Vital System, Revision 41
61058, Logic Diagram Engineered Safety Features Actuation System Unit 1, Revision 36 61022sh0001, Single Line Diagram 120V AC Vital Systems, Revision 51 61030, Single Line Diagram Vital 120V AC & 125V DC Emergency 250V DC FSAR Fig. No. 8-5, Revision 32
63024, Single Line Diagram 125V DC Vital System Bus 21, Revision 38 61005, Meter and Relay Diagram 4KV System Unit Buses 11 and 14 FSAR Fig No.8-4, Revision 36
61025, Single Line Diagram 125V DC Vital System Buses 12 and 22, Revision 31
61024, Single Line Diagram 125V DC Vital System Bus 11, Revision 52

Miscellaneous

CCNPP Utilities Service Alliance Nuclear Safety Culture Assessment, dated August 2011 CCNPP Utilities Service Alliance Nuclear Safety Culture Assessment, dated August 2013
OI-43C, Unit 2 Main Turbine Performance Evaluation Checks, Rev 20
NO-1-203, Operations Performance Evaluation Requirements, RT 2-98-4-O-M, Rev 4 Shift Turnover Information Sheets dated 09/12/13 and 09/25/13
Attachment Security Maintenance Request for Period 01/01/13 through 09/12/13 Agenda - Condition Report and OE Screening Committee dated 09/10/13
Agenda - Management Review Committee dated 09/11/13 and 09/25/13 Quarterly Operations Aggregate Impact Assessment, July 2013 Part 21 Report 2002-10, Inadequate electric motor winding slot fill, Revisions 1 & 2 Regulatory Guide 1.52, Design, Testing, and Maintenance Criteria for Post Accident Engineered-Safety-Feature Atmosphere Cleanup System Air Filtration and Adsorption Units of Light-Water-Cooled Nuclear Power Plants, Revision 2, March 1978 Purchase Order
421690, Containment Air Cooler and Iodine Removal Unit Motors
EPRI Technical Report, Closed Cooling Water Chemistry Guideline, Revision 1 ANSI N41.12-1975, IEEE Standards Criteria for Class 1E Power Systems for Nuclear Power Generating Stations, March 14, 1975 EP EAL Upgrade to
NEI 99-01, Rev 5, as MRC approved on 9/23/2013 EP Department Health Indicator for 2012-2013 PQA Audit
EPP-13-01-C, Emergency Preparedness Program, dated 2/14/2013, Revision 0
SA-2012-000046, Maintenance Rule (a)(3) Self-Assessment for
Nov 2010-Oct 2012, Rev 0
SA- 2012-000090, Maintenance Self-Assessment on Supervisor Training, Revision 0
Maintenance Rule Program Health Report for 1/1/2013-3/31/2013, Revision 0
Maintenance Department Excellence Plan for 2013, Revision 0 Maintenance Corrective Action Program Health Report for August 2013, Revision 0
Attachment

LIST OF ACRONYMS

ACE Apparent Cause Evaluation
ADAMS Agency-Wide Documents Access and Management System
CAP Corrective Action Program
CCA Common Cause Analysis
CCNPP Calvert Cliffs Nuclear Power Plant
CFR Code of Federal Regulations
CR Condition Report
CRSC Condition Report Screening Committee
ECP Employee Concerns Program
MRC Management Review Committee
NRC Nuclear Regulatory Commission
OE Operating Experience
PARS Publicly Available Records
RCA Root Cause Analysis
SCWE Safety Conscious Work Environment

SDP Significance Determination Process

VDC Volts Direct Current