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{{#Wiki_filter:April 17, 2003
{{#Wiki_filter:April 17, 2003
Joseph E. Venable
Joseph E. Venable
Vice President Operations
Vice President Operations  
Waterford 3
Waterford 3
Entergy Operations, Inc.
Entergy Operations, Inc.
17265 River Road
17265 River Road
Killona, Louisiana 70066-0751
Killona, Louisiana 70066-0751
SUBJECT: NRC INSPECTION REPORT 50-382/03-04
SUBJECT: NRC INSPECTION REPORT 50-382/03-04  
Dear Mr. Venable:
Dear Mr. Venable:
On March 22, 2003, the NRC completed an inspection at your Waterford Steam Electric
On March 22, 2003, the NRC completed an inspection at your Waterford Steam Electric
Station, Unit 3. The enclosed report documents the inspection findings, which were discussed
Station, Unit 3. The enclosed report documents the inspection findings, which were discussed
on March 24, 2003, with you and other members of your staff.
on March 24, 2003, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
compliance with the Commissions rules and regulations and with the conditions of your license.  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
personnel.  
Based on the results of this inspection, one self-revealing finding was identified that was
Based on the results of this inspection, one self-revealing finding was identified that was
evaluated under the risk significance determination process as having very low safety
evaluated under the risk significance determination process as having very low safety
significance (Green). Additionally, a licensee identified violation is listed in Section 4OA7 of this
significance (Green). Additionally, a licensee identified violation is listed in Section 4OA7 of this
report. If you contest this noncited violation, you should provide a response within 30 days of
report. If you contest this noncited violation, you should provide a response within 30 days of
the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory
the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory
Commission, ATTN: Document Control Desk, Washington DC 20555-0001; and the NRC
Commission, ATTN: Document Control Desk, Washington DC 20555-0001; and the NRC
Line 43: Line 43:
enclosure, and your response will be made available electronically for public inspection in the
enclosure, and your response will be made available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                              Sincerely,
Sincerely,  
                                                      /RA/
/RA/
                                              William B. Jones
William B. Jones
                                              Project Branch E
Project Branch E
                                              Division of Reactor Projects
Division of Reactor Projects


Entergy Operations, Inc.           -2-
Entergy Operations, Inc.
Docket: 50-382
-2-
License: NPF-38
Docket:   50-382
License: NPF-38
Enclosure:
Enclosure:
NRC Inspection Report
NRC Inspection Report
50-382/03-04
  50-382/03-04
cc w/enclosure:
cc w/enclosure:
Executive Vice President and
Executive Vice President and  
Chief Operating Officer
  Chief Operating Officer
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, Mississippi 39286-1995
Jackson, Mississippi 39286-1995
Vice President, Operations Support
Vice President, Operations Support
Entergy Operations, Inc.
Entergy Operations, Inc.
P.O. Box 31995
P.O. Box 31995
Jackson, Mississippi 39286-1995
Jackson, Mississippi 39286-1995
Wise, Carter, Child & Caraway
Wise, Carter, Child & Caraway
P.O. Box 651
P.O. Box 651
Jackson, Mississippi 39205
Jackson, Mississippi 39205
General Manager, Plant Operations
General Manager, Plant Operations
Waterford 3 SES
Waterford 3 SES
Entergy Operations, Inc.
Entergy Operations, Inc.
17265 River Road
17265 River Road
Killona, Louisiana 70066-0751
Killona, Louisiana 70066-0751
Manager - Licensing Manager
Manager - Licensing Manager
Waterford 3 SES
Waterford 3 SES
Entergy Operations, Inc.
Entergy Operations, Inc.
17265 River Road
17265 River Road
Killona, Louisiana 70066-0751
Killona, Louisiana 70066-0751
Chairman
Chairman
Louisiana Public Service Commission
Louisiana Public Service Commission
P.O. Box 91154
P.O. Box 91154
Baton Rouge, Louisiana 70821-9154
Baton Rouge, Louisiana 70821-9154
Director, Nuclear Safety &
Director, Nuclear Safety &  
Regulatory Affairs
  Regulatory Affairs
Waterford 3 SES
Waterford 3 SES
Entergy Operations, Inc.
Entergy Operations, Inc.
17265 River Road
17265 River Road
Killona, Louisiana 70066-0751
Killona, Louisiana 70066-0751


Entergy Operations, Inc.           -3-
Entergy Operations, Inc.
-3-
Michael E. Henry, Administrator
Michael E. Henry, Administrator
and State Liaison Officer
  and State Liaison Officer
Department of Environmental Quality
Department of Environmental Quality
P.O. Box 82135
P.O. Box 82135
Baton Rouge, Louisiana 70884-2135
Baton Rouge, Louisiana 70884-2135
Parish President
Parish President  
St. Charles Parish
St. Charles Parish
P.O. Box 302
P.O. Box 302
Hahnville, Louisiana 70057
Hahnville, Louisiana 70057
Winston & Strawn
Winston & Strawn
1400 L Street, N.W.
1400 L Street, N.W.
Washington, D.C. 20005-3502
Washington, D.C. 20005-3502
Technological Services
Technological Services
  Branch Chief
  Branch Chief
FEMA Region VI
FEMA Region VI
800 North Loop 288
800 North Loop 288
Federal Regional Center
Federal Regional Center
Denton, Texas 76201-3698
Denton, Texas 76201-3698


Entergy Operations, Inc.                         -4-
Entergy Operations, Inc.
-4-
Electronic distribution by RIV:
Electronic distribution by RIV:
Regional Administrator (EWM)
Regional Administrator (EWM)
Line 125: Line 128:
W. A. Maier, RSLO (WAM)
W. A. Maier, RSLO (WAM)
Dale Thatcher (DFT)
Dale Thatcher (DFT)
ADAMS: * Yes            * No        Initials: ______
ADAMS:  Yes
* Publicly Available * Nonpublicly Available         * Sensitive * Nonsensitive
  No           Initials: ______  
R:\_WAT\2003\WT2003-04RP-MCH.wpd
Publicly Available Nonpublicly Available
RIV:RI:DRP/E           SRI:DRP/E         C:DRS/EMB     C:DRS/PSB     C:DRP/E
Sensitive
GFLarkin               MCHay             CSMarschall   TWPruett       WBJones
Nonsensitive
T - VGGaddy             T - VGGaddy           /RA/       E - MPShannon   /RA/
R:\\_WAT\\2003\\WT2003-04RP-MCH.wpd
4/11/03                 4/11/03           4/11/03       4/9/03         4/17/03
RIV:RI:DRP/E
OFFICIAL RECORD COPY                                   T=Telephone     E=E-mail F=Fax
SRI:DRP/E
C:DRS/EMB
C:DRS/PSB
C:DRP/E
GFLarkin
MCHay
CSMarschall
TWPruett
WBJones
T - VGGaddy
T - VGGaddy
      /RA/
  E - MPShannon     /RA/
4/11/03
4/11/03
4/11/03
4/9/03
4/17/03
OFFICIAL RECORD COPY
T=Telephone           E=E-mail       F=Fax


                                ENCLOSURE
ENCLOSURE
              U.S. NUCLEAR REGULATORY COMMISSION
U.S. NUCLEAR REGULATORY COMMISSION  
                                REGION IV
REGION IV  
Docket:     50-382
Docket:
License:     NPF-38
50-382  
Report:     50-382/03-04
License:
Licensee:   Entergy Operations, Inc.
NPF-38
Facility:   Waterford Steam Electric Station, Unit 3
Report:
Location:   Hwy. 18
50-382/03-04
            Killona, Louisiana
Licensee:
Dates:       December 29, 2002, through March 22, 2003
Entergy Operations, Inc.
Inspectors: M. C. Hay, Senior Resident Inspector
Facility:
            G. F. Larkin, Resident Inspector
Waterford Steam Electric Station, Unit 3
            J. M. Mateychick, Reactor Inspector
Location:
            P. A. Goldberg, Senior Reactor Inspector
Hwy. 18  
            Paul J. Elkmann, Emergency Preparedness Inspector
Killona, Louisiana
Approved By: W. B. Jones, Chief, Project Branch E
Dates:
Attachment: Supplemental Information
December 29, 2002, through March 22, 2003
Inspectors:
M. C. Hay, Senior Resident Inspector
G. F. Larkin, Resident Inspector
J. M. Mateychick, Reactor Inspector
P. A. Goldberg, Senior Reactor Inspector
Paul J. Elkmann, Emergency Preparedness Inspector
Approved By:
W. B. Jones, Chief, Project Branch E
Attachment:
Supplemental Information


                                      SUMMARY OF FINDINGS
SUMMARY OF FINDINGS
                                Waterford Steam Electric Station, Unit 3
Waterford Steam Electric Station, Unit 3
                                NRC Inspection Report 50-382/03-04
NRC Inspection Report 50-382/03-04
IR05000382/2003-04; Entergy Operations, Inc.; on 12/29/2002-03/22/2003; Waterford Steam
IR05000382/2003-04; Entergy Operations, Inc.; on 12/29/2002-03/22/2003; Waterford Steam
Electric Station; Unit 3; Event Followup
Electric Station; Unit 3; Event Followup
The report covered a 12-week period of inspection by resident inspectors, an emergency
The report covered a 12-week period of inspection by resident inspectors, an emergency
preparedness inspector, and a reactor inspector. The inspection identified one Green finding.
preparedness inspector, and a reactor inspector. The inspection identified one Green finding.  
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not
IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not
apply may be Green or be assigned a severity level after NRC management review. The
apply may be Green or be assigned a severity level after NRC management review. The
NRCs program for overseeing the safe operation of commercial nuclear power reactors is
NRCs program for overseeing the safe operation of commercial nuclear power reactors is
described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.     Inspector Identified and Self-Revealing Findings
A.
Cornerstone: Initiating Events
Inspector Identified and Self-Revealing Findings
        *       Green. A self-revealing finding was identified for the failure to maintain and
Cornerstone: Initiating Events
                operate main generator seal oil backup differential pressure regulating
*
                Valve SO-308 in accordance with vendor recommendations. This condition
Green. A self-revealing finding was identified for the failure to maintain and
                resulted in a turbine trip and subsequent reactor power cutback on
operate main generator seal oil backup differential pressure regulating
                February 14, 2003.
Valve SO-308 in accordance with vendor recommendations. This condition
                This self-revealing finding is greater than minor because it resulted in a
resulted in a turbine trip and subsequent reactor power cutback on
                perturbation in plant stability resulting in a reactor power cutback, similar to
February 14, 2003.
                example 4.b in Appendix E of Manual Chapter 0612. The finding is of very low
This self-revealing finding is greater than minor because it resulted in a
                safety significance because, although it caused a plant transient, it did not
perturbation in plant stability resulting in a reactor power cutback, similar to
                increase the likelihood of a primary or secondary system loss-of-coolant accident
example 4.b in Appendix E of Manual Chapter 0612. The finding is of very low
                initiator, did not contribute to the loss of mitigation equipment functions, and did
safety significance because, although it caused a plant transient, it did not
                not increase the likelihood of a fire or internal/external flood (Section 4OA3).
increase the likelihood of a primary or secondary system loss-of-coolant accident
B.     Licensee-Identified Violations
initiator, did not contribute to the loss of mitigation equipment functions, and did
        A violation of very low safety significance, which was identified by the licensee, was
not increase the likelihood of a fire or internal/external flood (Section 4OA3).
        reviewed by the inspectors. Corrective actions taken or planned by the licensee have
B.
        been entered into the licensee's corrective action program. The violation and corrective
Licensee-Identified Violations
        action tracking number is listed in Section 4OA7.
A violation of very low safety significance, which was identified by the licensee, was  
reviewed by the inspectors. Corrective actions taken or planned by the licensee have
been entered into the licensee's corrective action program. The violation and corrective
action tracking number is listed in Section 4OA7.


                                            Report Details
Report Details
Summary of Plant Status: The plant was operated at approximately 100 percent power
Summary of Plant Status: The plant was operated at approximately 100 percent power
December 29, 2002, through February 14, 2003. Power was reduced to approximately
December 29, 2002, through February 14, 2003. Power was reduced to approximately
60 percent power February 14, 2003, following a turbine trip and subsequent reactor power
60 percent power February 14, 2003, following a turbine trip and subsequent reactor power
cutback. The reactor was shutdown February 15, 2003, to support main turbine generator
cutback. The reactor was shutdown February 15, 2003, to support main turbine generator
repairs. On February 19, 2003, reactor power was restored to 100 percent. Reactor power
repairs. On February 19, 2003, reactor power was restored to 100 percent. Reactor power
was maintained at approximately 100 percent throughout the remainder of the inspection
was maintained at approximately 100 percent throughout the remainder of the inspection
period.
period.
1       REACTOR SAFETY
1
REACTOR SAFETY
Initiating Events, Mitigating Systems, Barrier Integrity (R)
Initiating Events, Mitigating Systems, Barrier Integrity (R)
1R01 Adverse Weather Protection (71111.01)
1R01
  a.     Inspection Scope
Adverse Weather Protection (71111.01)
        On January 23, 2003, the inspectors performed a walkdown of components and
  a.
        systems susceptible to freezing using Procedure OP-002-007, Freeze Protection and
Inspection Scope
        Temperature Maintenance, Revision 10, to verify that the onset of cold weather would
On January 23, 2003, the inspectors performed a walkdown of components and
        not affect mitigating systems. This inspection included a review of deficiency tags and
systems susceptible to freezing using Procedure OP-002-007, Freeze Protection and
        condition reports associated with heat tracing and other cold weather protection
Temperature Maintenance, Revision 10, to verify that the onset of cold weather would
        measures to determine their impact on the systems. Additionally, the inspectors
not affect mitigating systems. This inspection included a review of deficiency tags and
        discussed adverse weather preparations with various licensee personnel.
condition reports associated with heat tracing and other cold weather protection
  b.     Findings
measures to determine their impact on the systems. Additionally, the inspectors
        No findings of significance were identified.
discussed adverse weather preparations with various licensee personnel.
1R04 Equipment Alignment (71111.04)
  b.
  .1     Reactor Auxiliary Building Cable Vault and Switchgear Area Ventilation System
Findings
  a.     Inspection Scope
No findings of significance were identified.
        The inspectors performed a complete equipment alignment inspection of the reactor
1R04
        auxiliary building cable vault and switchgear area ventilation system. A review of select
Equipment Alignment (71111.04)
        maintenance work orders and corrective action documents was performed to assess the
  .1
        material condition and performance of the switchgear area ventilation system. System
Reactor Auxiliary Building Cable Vault and Switchgear Area Ventilation System
        configuration was assessed using Operating Procedure OP-003-026, "Cable Vault and
  a.
        Switchgear HVAC," Revision 7. A walkdown of accessible portions of the system was
Inspection Scope
        performed to assess material condition, such as system leaks and housekeeping issues,
The inspectors performed a complete equipment alignment inspection of the reactor
        that could adversely affect system operability. The inspection also consisted of verifying
auxiliary building cable vault and switchgear area ventilation system. A review of select
        that the system was installed, maintained, and tested as described in the Updated Final
maintenance work orders and corrective action documents was performed to assess the
        Safety Analysis Report and Technical Specifications.
material condition and performance of the switchgear area ventilation system. System
  b.     Findings
configuration was assessed using Operating Procedure OP-003-026, "Cable Vault and
        Introduction: The NRC identified that Switchgear Ventilation System Trains A and B
Switchgear HVAC," Revision 7. A walkdown of accessible portions of the system was
        safety-related outside air intake Dampers SVS-101 and SVS-102, respectively, are
performed to assess material condition, such as system leaks and housekeeping issues,
that could adversely affect system operability. The inspection also consisted of verifying
that the system was installed, maintained, and tested as described in the Updated Final
Safety Analysis Report and Technical Specifications.
  b.
Findings
Introduction: The NRC identified that Switchgear Ventilation System Trains A and B
safety-related outside air intake Dampers SVS-101 and SVS-102, respectively, are


                                          -2-
-2-
susceptible to a common mode failure vulnerability associated with a loss of
susceptible to a common mode failure vulnerability associated with a loss of
nonsafety-related instrument air. Pending determination of the findings safety
nonsafety-related instrument air. Pending determination of the findings safety
significance, this finding is identified as Unresolved Item (URI) 50-382/03-04-01.
significance, this finding is identified as Unresolved Item (URI) 50-382/03-04-01.
Description: Switchgear Ventilation System Trains A and B outside air intake
Description: Switchgear Ventilation System Trains A and B outside air intake
Dampers SVS-101 and SVS-102, respectively, are safety-related, installed in series,
Dampers SVS-101 and SVS-102, respectively, are safety-related, installed in series,
and pneumatically operated. A safety injection actuation signal automatically positions
and pneumatically operated. A safety injection actuation signal automatically positions
these dampers to a minimum open position using instrument air. The inspectors noted
these dampers to a minimum open position using instrument air. The inspectors noted
that a loss of instrument air, which is a nonsafety-related system, would introduce a
that a loss of instrument air, which is a nonsafety-related system, would introduce a
common mode failure for Dampers SVS-101 and SVS-102 preventing these valves from
common mode failure for Dampers SVS-101 and SVS-102 preventing these valves from
performing their safety-related function during certain postaccident conditions. In
performing their safety-related function during certain postaccident conditions. In
response to this concern, the licensee took immediate corrective actions and gagged, in
response to this concern, the licensee took immediate corrective actions and gagged, in
the minimum open position, Damper SVS-102. A review of design documentation by
the minimum open position, Damper SVS-102. A review of design documentation by
the inspectors and the licensee identified that the basis for the valves being positioned
the inspectors and the licensee identified that the basis for the valves being positioned
in the minimum open position following a safety injection actuation signal was not clearly
in the minimum open position following a safety injection actuation signal was not clearly
documented. The licensee developed, but had yet to implement, a special test to
documented. The licensee developed, but had yet to implement, a special test to
assess the effects on the control room envelope and those areas surrounding the
assess the effects on the control room envelope and those areas surrounding the
control room due to Dampers SVS-101 and SVS-102 failing in the open position.
control room due to Dampers SVS-101 and SVS-102 failing in the open position.
Analysis: Using the guidance in Appendix B of Inspection Manual Chapter 0612, this
Analysis: Using the guidance in Appendix B of Inspection Manual Chapter 0612, this
issue potentially will screen more than minor. The barrier integrity objective, to provide
issue potentially will screen more than minor. The barrier integrity objective, to provide
reasonable assurance that the physical design barriers to protect the control room
reasonable assurance that the physical design barriers to protect the control room
operators from radionuclide releases caused by accidents or events, was affected.
operators from radionuclide releases caused by accidents or events, was affected.  
A Phase 1 screening was performed for the issue utilizing NRC Manual Chapter 0609,
A Phase 1 screening was performed for the issue utilizing NRC Manual Chapter 0609,
Appendix A, Attachment 1. The finding was assessed as potentially affecting the
Appendix A, Attachment 1. The finding was assessed as potentially affecting the
radiological barrier function for the control room. The significance of this issue is
radiological barrier function for the control room. The significance of this issue is
unresolved pending the results of a special test that will determine the pressure effects
unresolved pending the results of a special test that will determine the pressure effects
on the control room envelope following failure of Dampers SVS-101 and SVS-102 to
on the control room envelope following failure of Dampers SVS-101 and SVS-102 to
maintain their minimum open safety position following a safety injection actuation signal.
maintain their minimum open safety position following a safety injection actuation signal.  
Enforcement: 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in
Enforcement: 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in
part, that Measures shall be established to assure that applicable regulatory
part, that Measures shall be established to assure that applicable regulatory
requirements and the design basis are correctly translated into specifications, drawings,
requirements and the design basis are correctly translated into specifications, drawings,
procedures, and instructions. The failure to maintain design control of the switchgear
procedures, and instructions. The failure to maintain design control of the switchgear
ventilation system resulting in the potential common mode failure of Dampers SVS-101
ventilation system resulting in the potential common mode failure of Dampers SVS-101
and SVS-102, due to loss of the nonsafety related instrument air system, is being
and SVS-102, due to loss of the nonsafety related instrument air system, is being
considered a violation of 10 CFR Part 50, Appendix B, Criterion III. Pending
considered a violation of 10 CFR Part 50, Appendix B, Criterion III. Pending
determination of the findings safety significance, this finding is identified as
determination of the findings safety significance, this finding is identified as
URI 50-382/03-04-01. The licensee documented this issue in their corrective action
URI 50-382/03-04-01. The licensee documented this issue in their corrective action
process as Condition Report CR-WF3-2003-0062.
process as Condition Report CR-WF3-2003-0062.


                                            -3-
-3-
.2 High-Pressure Safety Injection System Train A
  .2
a. Inspection Scope
High-Pressure Safety Injection System Train A
  On February 4, 2003, the inspectors performed a partial walkdown of the mechanical
  a.
  and electrical components of a critical portion of High-Pressure Safety Injection System
Inspection Scope
  Train A while the train was in a standby alignment. This walkdown was completed
On February 4, 2003, the inspectors performed a partial walkdown of the mechanical
  during scheduled maintenance that rendered Train B inoperable. The inspectors
and electrical components of a critical portion of High-Pressure Safety Injection System
  verified that the system was installed, maintained, and tested as described in the
Train A while the train was in a standby alignment. This walkdown was completed
  Updated Final Safety Analysis Report and Technical Specifications.
during scheduled maintenance that rendered Train B inoperable. The inspectors
b. Findings
verified that the system was installed, maintained, and tested as described in the
  No findings of significance were identified.
Updated Final Safety Analysis Report and Technical Specifications.
.3 Shield Building Ventilation System
  b.
a. Inspection Scope
Findings
  On January 29, 2003, the inspectors performed a partial walkdown of the mechanical
No findings of significance were identified.
  and electrical components of a critical portion of Shield Building Ventilation System
  .3
  Train A. This walkdown was completed during scheduled maintenance that rendered
Shield Building Ventilation System
  Train B inoperable. The inspectors verified that the system was installed, maintained,
  a.
  and tested as described in the Updated Final Safety Analysis Report and Technical
Inspection Scope
  Specifications.
On January 29, 2003, the inspectors performed a partial walkdown of the mechanical
b. Findings
and electrical components of a critical portion of Shield Building Ventilation System
  No findings of significance were identified.
Train A. This walkdown was completed during scheduled maintenance that rendered
.4 Component Cooling Water Train A
Train B inoperable. The inspectors verified that the system was installed, maintained,
a. Inspection Scope
and tested as described in the Updated Final Safety Analysis Report and Technical
  On March 13, 2003, the inspectors completed a partial equipment alignment inspection
Specifications.
  of Component Cooling Water Train A. A review of select maintenance work orders and
  b.
  corrective action documents was performed to assess the material condition and
Findings
  performance of Component Cooling Water Train A. System configuration was assessed
No findings of significance were identified.
  using Operating Procedure OP-002-003, "Component Cooling Water," Revision 13. A
  .4
  walkdown of accessible portions of the system was performed to assess material
Component Cooling Water Train A
  condition, such as system leaks and housekeeping issues, that could adversely affect
  a.
  system operability.
Inspection Scope
b. Findings
On March 13, 2003, the inspectors completed a partial equipment alignment inspection
  No findings of significance were identified.
of Component Cooling Water Train A. A review of select maintenance work orders and
corrective action documents was performed to assess the material condition and
performance of Component Cooling Water Train A. System configuration was assessed
using Operating Procedure OP-002-003, "Component Cooling Water," Revision 13. A
walkdown of accessible portions of the system was performed to assess material
condition, such as system leaks and housekeeping issues, that could adversely affect
system operability.
  b.
Findings
No findings of significance were identified.


                                              -4-
-4-
1R05 Fire Protection (71111.05)
1R05
    The inspectors conducted six inspections to determine if the licensee had implemented
Fire Protection (71111.05)
    a fire protection program that adequately controlled combustibles and ignition sources
The inspectors conducted six inspections to determine if the licensee had implemented
    within the plant, effectively maintained fire detection and suppression capabilities, and
a fire protection program that adequately controlled combustibles and ignition sources
    maintained passive fire protection features in good material condition.
within the plant, effectively maintained fire detection and suppression capabilities, and
    The following areas were inspected:
maintained passive fire protection features in good material condition.
    *       Reactor auxiliary building +21-foot elevation on January 23, 2003
The following areas were inspected:
    *       Control room envelop on February 4, 2003
*
    *       Safety Injection Pump Area B on February 4, 2003
Reactor auxiliary building +21-foot elevation on January 23, 2003
    *       Switchgear Room B on February 4, 2003
*
    *       Reactor auxiliary building +46-foot elevation on February 20, 2003
Control room envelop on February 4, 2003
    *       Reactor auxiliary building -4-foot and -35-foot elevations on February 28, 2003
*
b. Findings
Safety Injection Pump Area B on February 4, 2003
    No findings of significance were identified.
*
1R11 Licensed Operator Requalification (71111.11)
Switchgear Room B on February 4, 2003
a. Inspection Scope
*
    On February 3, 2003, the inspectors observed licensed operator simulator training. The
Reactor auxiliary building +46-foot elevation on February 20, 2003
    simulator training evaluated the operator's ability to recognize, diagnose, and respond to
*
    a small tube leak in Steam Generator 1, a reactor trip with failure of two control element
Reactor auxiliary building -4-foot and -35-foot elevations on February 28, 2003
    assemblies to insert, and the failure of High-Pressure Safety Injection Pump B to start
  b.
    on a safety injection actuation signal. The inspectors observed and evaluated the
Findings
    following areas:
No findings of significance were identified.
    *       Understanding and interpreting annunciator and alarm signals
1R11
    *       Diagnosing events and conditions based on signals or readings
Licensed Operator Requalification (71111.11)
    *       Understanding plant systems
  a.
    *       Use and adherence of Technical Specifications
Inspection Scope
    *       Crew communications including command and control
On February 3, 2003, the inspectors observed licensed operator simulator training. The
    *       The crew's and evaluator's critiques
simulator training evaluated the operator's ability to recognize, diagnose, and respond to
b. Findings
a small tube leak in Steam Generator 1, a reactor trip with failure of two control element
    No findings of significance were identified.
assemblies to insert, and the failure of High-Pressure Safety Injection Pump B to start
on a safety injection actuation signal. The inspectors observed and evaluated the
following areas:
*
Understanding and interpreting annunciator and alarm signals
*
Diagnosing events and conditions based on signals or readings
*
Understanding plant systems
*
Use and adherence of Technical Specifications
*
Crew communications including command and control
*
The crew's and evaluator's critiques
  b.
Findings
No findings of significance were identified.


                                              -5-
-5-
1R12 Maintenance Rule Implementation (71111.12)
1R12
.1 Routine Maintenance Rule Review
Maintenance Rule Implementation (71111.12)
a. Inspection Scope
  .1
    During the inspection period, the inspectors reviewed licensee implementation of the
Routine Maintenance Rule Review
    Maintenance Rule. The inspectors considered the characterization, safety significance,
  a.
    performance criteria, and appropriateness of goals and corrective actions. The
Inspection Scope
    inspectors assessed the licensees implementation of the Maintenance Rule to the
During the inspection period, the inspectors reviewed licensee implementation of the
    requirements outlined in 10 CFR 50.65 and Regulatory Guide 1.160, Monitoring the
Maintenance Rule. The inspectors considered the characterization, safety significance,
    Effectiveness of Maintenance at Nuclear Power Plants, Revision 2. The inspectors
performance criteria, and appropriateness of goals and corrective actions. The
    reviewed the following systems that displayed performance problems:
inspectors assessed the licensees implementation of the Maintenance Rule to the
    *       Emergency Diesel Generating System Train A
requirements outlined in 10 CFR 50.65 and Regulatory Guide 1.160, Monitoring the
    *       Containment Cooling HVAC Trains A and B
Effectiveness of Maintenance at Nuclear Power Plants, Revision 2. The inspectors
b. Findings
reviewed the following systems that displayed performance problems:
    No findings of significance were identified.
*
.2 Periodic Evaluation Reviews
Emergency Diesel Generating System Train A
a. Inspection Scope
*
    The inspectors reviewed the Waterford 3 report documenting the performance of the
Containment Cooling HVAC Trains A and B  
    last Maintenance Rule periodic effectiveness assessment. This periodic evaluation
  b.
    covered the period from November 2000 through April 2002.
Findings
    The inspectors reviewed the program for monitoring risk-significant functions associated
No findings of significance were identified.
    with structures, systems, and components using reliability and unavailability. The
  .2
    performance monitoring of nonrisk-significant functions using plant level criteria was
Periodic Evaluation Reviews
    also reviewed.
  a.
    The inspectors evaluated whether the report contained adequate assessment of the
Inspection Scope
    performance of the Maintenance Rule Program as well as conformance with applicable
The inspectors reviewed the Waterford 3 report documenting the performance of the
    programmatic and regulatory requirements. To accomplish this, the inspectors verified
last Maintenance Rule periodic effectiveness assessment. This periodic evaluation
    that the licensee appropriately and correctly addressed the following attributes in the
covered the period from November 2000 through April 2002.
    assessment reports:
The inspectors reviewed the program for monitoring risk-significant functions associated
    *       The program treatment of nonrisk-significant structure, system, and component
with structures, systems, and components using reliability and unavailability. The
            functions monitored against plant level performance criteria
performance monitoring of nonrisk-significant functions using plant level criteria was
    *       Program adjustments made in response to unbalanced reliability and availability
also reviewed.
    *       The application of industry operating experience
The inspectors evaluated whether the report contained adequate assessment of the
performance of the Maintenance Rule Program as well as conformance with applicable
programmatic and regulatory requirements. To accomplish this, the inspectors verified
that the licensee appropriately and correctly addressed the following attributes in the
assessment reports:
*
The program treatment of nonrisk-significant structure, system, and component  
functions monitored against plant level performance criteria
*
Program adjustments made in response to unbalanced reliability and availability
*
The application of industry operating experience


                                            -6-
-6-
  *       Performance review of Category (a)(1) systems
*
  *       Evaluation of the bases for system category status change (e.g., (a)(1) to (a)(2)
Performance review of Category (a)(1) systems
            or (a)(2) to (a)(1))
*
  *       Effectiveness of performance and condition monitoring at component, train,
Evaluation of the bases for system category status change (e.g., (a)(1) to (a)(2)
            system, and plant levels
or (a)(2) to (a)(1))
  *       Review and adjustment of definitions of functional failures
*
  The inspector also verified that the issuance of the two most recent assessments met
Effectiveness of performance and condition monitoring at component, train,
  the regulatory timeliness requirements.
system, and plant levels
  The inspectors reviewed procedures, condition reports, and Category (a)(1) recovery
*
  plans associated with the above activities for the following systems: core protection
Review and adjustment of definitions of functional failures
  calculator, emergency diesel generator sequencer, feedwater, broad range gas
The inspector also verified that the issuance of the two most recent assessments met
  monitors, process radiation monitors, essential chillers (refrigeration), and shutdown
the regulatory timeliness requirements.
  cooling.
The inspectors reviewed procedures, condition reports, and Category (a)(1) recovery
b. Findings
plans associated with the above activities for the following systems: core protection
  No findings of significance were identified.
calculator, emergency diesel generator sequencer, feedwater, broad range gas
.3 Identification and Resolution of Problems
monitors, process radiation monitors, essential chillers (refrigeration), and shutdown
a. Inspection Scope
cooling.
  The inspectors evaluated the use of the corrective action system within the Maintenance
  b.
  Rule Program for issues associated with risk-significant systems. The inspectors
Findings
  examined a sample of corrective action documents associated with systems which were,
No findings of significance were identified.
  or had been, in Maintenance Rule Category (a)(1), including recovery plans for
  .3
  improving the system performance. The inspectors performed this review to establish
Identification and Resolution of Problems
  that the corrective action program was entered at the appropriate threshold for the
  a.
  purpose of:
Inspection Scope
  *       Implementing the corrective action process when a performance criterion was
The inspectors evaluated the use of the corrective action system within the Maintenance
            exceeded
Rule Program for issues associated with risk-significant systems. The inspectors
  *       Correcting performance-related issues or conditions identified during the periodic
examined a sample of corrective action documents associated with systems which were,
            evaluation
or had been, in Maintenance Rule Category (a)(1), including recovery plans for
  *       Correcting generic issues or conditions identified during programmatic
improving the system performance. The inspectors performed this review to establish
            assessments, audits, or surveillances.
that the corrective action program was entered at the appropriate threshold for the
  The inspectors identified an observation concerning the licensee's implementation of
purpose of:
  appropriate corrective actions to maintain the performance of the core protection
*
  calculator system. The core protection calculator was placed in Maintenance Rule
Implementing the corrective action process when a performance criterion was
exceeded
*
Correcting performance-related issues or conditions identified during the periodic
evaluation
*
Correcting generic issues or conditions identified during programmatic
assessments, audits, or surveillances.
The inspectors identified an observation concerning the licensee's implementation of
appropriate corrective actions to maintain the performance of the core protection
calculator system. The core protection calculator was placed in Maintenance Rule


                                              -7-
-7-
    status Category (a)(1) from July 2000 to February 2001 and again in December 2001
status Category (a)(1) from July 2000 to February 2001 and again in December 2001
    until the time of this inspection due to both functional failures and unavailability.
until the time of this inspection due to both functional failures and unavailability.  
    The inspectors reviewed the licensees goals for monitoring the performance of the core
The inspectors reviewed the licensees goals for monitoring the performance of the core
    protection calculator for the Maintenance Rule. The inspectors noted that one
protection calculator for the Maintenance Rule. The inspectors noted that one
    performance criteria for each channel to remain in Category (a)(2) consisted of
performance criteria for each channel to remain in Category (a)(2) consisted of
    functional failures that resulted in a spurious channel trip being < 20 functional failures
functional failures that resulted in a spurious channel trip being < 20 functional failures
    per 18-month period per channel. The inspectors found that Channel D is not meeting
per 18-month period per channel. The inspectors found that Channel D is not meeting
    this goal. The inspectors review of system performance since July 1999 against this
this goal. The inspectors review of system performance since July 1999 against this
    goal indicated that prior to July 2000 there was another period when Channel D was not
goal indicated that prior to July 2000 there was another period when Channel D was not
    meeting the goal. In addition, the inspectors found that Channels B and C also had
meeting the goal. In addition, the inspectors found that Channels B and C also had
    periods of not meeting this goal, sometimes concurrently with Channel D. The licensee
periods of not meeting this goal, sometimes concurrently with Channel D. The licensee
    stated that since 1999 there were 13 instances where one channel was in trip and a
stated that since 1999 there were 13 instances where one channel was in trip and a
    second channel was in bypass.
second channel was in bypass.
    The inspectors reviewed Condition Reports CR-WF3-2000-0839 and -2001-1346 and
The inspectors reviewed Condition Reports CR-WF3-2000-0839 and -2001-1346 and
    found that the licensee's corrective actions were focused on replacing failed electronic
found that the licensee's corrective actions were focused on replacing failed electronic
    components and improving the ventilation flow through the core protection calculator
components and improving the ventilation flow through the core protection calculator
    cabinets to reduce the operating temperature of the electronic components. The
cabinets to reduce the operating temperature of the electronic components. The
    licensee intends to maintain the current core protection calculators system until
licensee intends to maintain the current core protection calculators system until
    replacement during Refueling Outage 14 in the fall of 2006.
replacement during Refueling Outage 14 in the fall of 2006.  
b. Findings
  b.
    No findings of significance were identified.
Findings
1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)
No findings of significance were identified.
a. Inspection Scope
1R13
    The inspectors reviewed risk assessments for planned or emergent maintenance
Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)
    activities to determine if the licensee met the requirements of 10 CFR 50.65(a)(4) for
  a.
    assessing and managing any increase in risk from these activities. Risk evaluations of
Inspection Scope
    the following five occurrences were reviewed:
The inspectors reviewed risk assessments for planned or emergent maintenance
    *       On January 23, 2003, Nitrogen Gas Valve NG-709 was declared inoperable and
activities to determine if the licensee met the requirements of 10 CFR 50.65(a)(4) for
              required emergent repairs.
assessing and managing any increase in risk from these activities. Risk evaluations of
    *       On February 5, 2003, Emergency Feedwater Pump B was declared inoperable
the following five occurrences were reviewed:
              and required emergent repairs.
*
    *       On February 6, 2003, troubleshooting activities were performed to isolate a
On January 23, 2003, Nitrogen Gas Valve NG-709 was declared inoperable and
              ground on the control element drive mechanism control system.
required emergent repairs.
    *       On February 9, 2003, Main Steam Admission Valve MS-401B to the
*
              turbine-driven auxiliary feedwater pump was declared inoperable and required
On February 5, 2003, Emergency Feedwater Pump B was declared inoperable
              emergent repairs.
and required emergent repairs.
*
On February 6, 2003, troubleshooting activities were performed to isolate a
ground on the control element drive mechanism control system.
*
On February 9, 2003, Main Steam Admission Valve MS-401B to the
turbine-driven auxiliary feedwater pump was declared inoperable and required
emergent repairs.


                                                -8-
-8-
    *       On March 14, 2003, the Plant Protection System Channel B High Log Power Trip
*
            Bypass Module was replaced.
On March 14, 2003, the Plant Protection System Channel B High Log Power Trip
b. Findings
Bypass Module was replaced.
    No findings of significance were identified.
  b.
1R14 Personnel Performance During Nonroutine Plant Evolutions (71111.14)
Findings
a. Inspection Scope
No findings of significance were identified.
    For the nonroutine events described below, the inspectors reviewed operator logs, plant
1R14
    computer data, and strip charts to determine what occurred, how the operators
Personnel Performance During Nonroutine Plant Evolutions (71111.14)
    responded, and whether the response was in accordance with plant procedures:
  a.
    *       On February 14, 2003, the inspectors observed the site response to a turbine trip
Inspection Scope
            followed by a reactor power cutback from 100 percent power. Reactor power
For the nonroutine events described below, the inspectors reviewed operator logs, plant
            was reduced to approximately 60 percent with the steam bypass control system
computer data, and strip charts to determine what occurred, how the operators
            available to mitigate the transient. On February 15, 2003, the inspectors
responded, and whether the response was in accordance with plant procedures:
            observed the operators perform a reactor shutdown following the identification of
*
            insulation degradation that affected the main generator exciter.
On February 14, 2003, the inspectors observed the site response to a turbine trip
b. Findings
followed by a reactor power cutback from 100 percent power. Reactor power
    No findings of significance were identified.
was reduced to approximately 60 percent with the steam bypass control system
1R15 Operability Evaluations (71111.15)
available to mitigate the transient. On February 15, 2003, the inspectors
a. Inspection Scope
observed the operators perform a reactor shutdown following the identification of
    The inspectors reviewed the technical adequacy of four operability evaluations to verify
insulation degradation that affected the main generator exciter.
    that they were sufficient to justify continued operation of a system or component. The
  b.
    inspectors considered that, although equipment was potentially degraded, the operability
Findings
    evaluation provided adequate justification that the equipment could still meet its
No findings of significance were identified.
    Technical Specification, Updated Final Safety Analysis Report, and design-bases
1R15
    requirements and that the potential risk increase contributed by the degraded equipment
Operability Evaluations (71111.15)
    was thoroughly evaluated. The following evaluations were reviewed:
  a.
    *       Operability evaluation addressing missing nuts, washers, and a U-bolt affecting
Inspection Scope
            the auxiliary component cooling water system Wet Cooling Tower A (Condition
The inspectors reviewed the technical adequacy of four operability evaluations to verify
            Report CR-WF3-2003-00089)
that they were sufficient to justify continued operation of a system or component. The
    *       Operability evaluation addressing broken reach rod linkage affecting operation of
inspectors considered that, although equipment was potentially degraded, the operability
            Containment Spray Valve CS-117B (Condition Report CR-WF3-2003-00309)
evaluation provided adequate justification that the equipment could still meet its
Technical Specification, Updated Final Safety Analysis Report, and design-bases
requirements and that the potential risk increase contributed by the degraded equipment
was thoroughly evaluated. The following evaluations were reviewed:
*
Operability evaluation addressing missing nuts, washers, and a U-bolt affecting
the auxiliary component cooling water system Wet Cooling Tower A (Condition
Report CR-WF3-2003-00089)
*
Operability evaluation addressing broken reach rod linkage affecting operation of
Containment Spray Valve CS-117B (Condition Report CR-WF3-2003-00309)


                                              -9-
-9-
    *       Operability evaluation addressing total component cooling water flow in the
*
            accident alignment exceeding design flow rates (Condition Report CR-WF3-2003-00512)
Operability evaluation addressing total component cooling water flow in the
    *       Operability evaluation addressing degraded seal water flow to Charging Pump B
accident alignment exceeding design flow rates (Condition Report CR-WF3-2003-00512)
            (Condition Report CR-WF3-2003-00640)
*
b. Findings
Operability evaluation addressing degraded seal water flow to Charging Pump B
    No findings of significance were identified.
(Condition Report CR-WF3-2003-00640)
1R16 Operator Workarounds (71111.16)
  b.
a. Inspection Scope
Findings
    The inspectors performed a review of operator workarounds. This review evaluated the
No findings of significance were identified.
    cumulative affects of current operator workarounds to assess the overall impact
1R16
    affecting the operators ability to respond in a correct and timely manner to plant
Operator Workarounds (71111.16)
    transients and accidents.
  a.
b. Findings
Inspection Scope
    No findings of significance were identified.
The inspectors performed a review of operator workarounds. This review evaluated the
1R19 Postmaintenance Testing (71111.19)
cumulative affects of current operator workarounds to assess the overall impact
a. Inspection Scope
affecting the operators ability to respond in a correct and timely manner to plant
    The inspectors reviewed postmaintenance tests to verify system operability and
transients and accidents.
    functional capabilities. The inspectors considered whether testing met design and
  b.
    licensing bases, Technical Specifications, and licensee procedural requirements. The
Findings
    inspectors reviewed the testing results for the following six components:
No findings of significance were identified.  
    *       Essential Chiller A following a low refrigerant pressure trip due to refrigerant
1R19
            leakage through a damaged dehydrator gasket joint on December 12, 2002
Postmaintenance Testing (71111.19)
    *       Nitrogen Gas Valve NG-811 following repair work on valve internal parts on
  a.
            February 20, 2003
Inspection Scope
    *       Nitrogen Gas Valve NG-709 following valve stroke failure on February 23, 2003
The inspectors reviewed postmaintenance tests to verify system operability and
    *       Chilled Water Valve CHW-900 following valve actuator maintenance on
functional capabilities. The inspectors considered whether testing met design and
            February 25, 2003
licensing bases, Technical Specifications, and licensee procedural requirements. The
    *       Main Steam Valve MS-401B following motor replacement on March 10, 2003
inspectors reviewed the testing results for the following six components:
    *       Plant Protection System Channel B High Log Power Trip Bypass Module
*
            following replacement on March 14, 2003
Essential Chiller A following a low refrigerant pressure trip due to refrigerant
leakage through a damaged dehydrator gasket joint on December 12, 2002
*
Nitrogen Gas Valve NG-811 following repair work on valve internal parts on
February 20, 2003
*
Nitrogen Gas Valve NG-709 following valve stroke failure on February 23, 2003
*
Chilled Water Valve CHW-900 following valve actuator maintenance on
February 25, 2003
*
Main Steam Valve MS-401B following motor replacement on March 10, 2003
*
Plant Protection System Channel B High Log Power Trip Bypass Module
following replacement on March 14, 2003


                                              -10-
-10-
b. Findings
  b.
    No findings of significance were identified.
Findings
1R22 Surveillance Testing (71111.22)
No findings of significance were identified.
a. Inspection Scope
1R22
    The inspectors observed or reviewed the following six surveillance tests to ensure the
Surveillance Testing (71111.22)
    systems were capable of performing their safety function and to assess their operational
  a.
    readiness. Specifically, the inspectors considered whether the following surveillance
Inspection Scope
    tests met Technical Specifications, the Updated Final Safety Analysis Report, and
The inspectors observed or reviewed the following six surveillance tests to ensure the
    licensee procedural requirements:
systems were capable of performing their safety function and to assess their operational
    *       Surveillance Procedure OP-903-030, Safety Injection Pump Operability
readiness. Specifically, the inspectors considered whether the following surveillance
            Verification, Revision 13, was reviewed on January 24, 2003. This surveillance
tests met Technical Specifications, the Updated Final Safety Analysis Report, and
            tested the functional capability of Low-Pressure Safety Injection Pump A.
licensee procedural requirements:
    *       Surveillance Procedure OP-903-046, Emergency Feedwater Pump Operability
*
            Check, Revision 15, performed on February 5, 2002. This surveillance tested
Surveillance Procedure OP-903-030, Safety Injection Pump Operability
            the functional capability of motor-driven Emergency Feedwater Pump B.
Verification, Revision 13, was reviewed on January 24, 2003. This surveillance
    *       Surveillance Procedure OP-903-107, Plant Protection System Channel
tested the functional capability of Low-Pressure Safety Injection Pump A.
            _A_B_C_D Functional Test, Revision 14, was reviewed on February 19, 2003.
*
            This surveillance tested the bypass, pretrip, and trip actuation capability of Plant
Surveillance Procedure OP-903-046, Emergency Feedwater Pump Operability
            Protection System Channel A.
Check, Revision 15, performed on February 5, 2002. This surveillance tested
    *       Surveillance Procedure STA-001-001, Containment Air Lock Seal Leakage
the functional capability of motor-driven Emergency Feedwater Pump B.
            Test, Revision 4, was reviewed on February 20, 2003. This surveillance tested
*
            the containment air lock pressure decay rate.
Surveillance Procedure OP-903-107, Plant Protection System Channel
    *       Surveillance Procedure OP-903-102, Safety Channel Nuclear Instrumentation
_A_B_C_D Functional Test, Revision 14, was reviewed on February 19, 2003.
            Functional Test, Revision 10, was reviewed on February 21, 2003. This
This surveillance tested the bypass, pretrip, and trip actuation capability of Plant
            surveillance tested the functional capability of the Excore Nuclear Safety
Protection System Channel A.
            Channels.
*
    *       Surveillance Procedure OP-903-043, Shield Building Ventilation System
Surveillance Procedure STA-001-001, Containment Air Lock Seal Leakage
            Operability Check, Revision 9, was reviewed on March 10, 2003. This
Test, Revision 4, was reviewed on February 20, 2003. This surveillance tested
            surveillance tested stroke times for critical valves required to change position
the containment air lock pressure decay rate.  
            and verified adequate flow rates through the filter media.
*
b. Findings
Surveillance Procedure OP-903-102, Safety Channel Nuclear Instrumentation
    No findings of significance were identified.
Functional Test, Revision 10, was reviewed on February 21, 2003. This
surveillance tested the functional capability of the Excore Nuclear Safety
Channels.
*
Surveillance Procedure OP-903-043, Shield Building Ventilation System
Operability Check, Revision 9, was reviewed on March 10, 2003. This
surveillance tested stroke times for critical valves required to change position
and verified adequate flow rates through the filter media.
  b.
Findings
No findings of significance were identified.


                                              -11-
-11-
1R23 Temporary Plant Modifications (71111.23)
1R23
a.   Inspection Scope
Temporary Plant Modifications (71111.23)
      The inspectors reviewed a temporary plant modification of the switchgear ventilation
  a.
      system to ensure that the modification did not adversely affect system operability or
Inspection Scope
      design requirements specified in the Updated Final Safety Analysis Report and
The inspectors reviewed a temporary plant modification of the switchgear ventilation
      Technical Specifications. The modification consisted of gagging switchgear ventilation
system to ensure that the modification did not adversely affect system operability or
      system Damper SVS-102 in the minimum open position. This modification was installed
design requirements specified in the Updated Final Safety Analysis Report and
      to place the damper in its fail safe position after identifying that a loss of
Technical Specifications. The modification consisted of gagging switchgear ventilation
      nonsafety-related instrument air would prevent the valve from performing its
system Damper SVS-102 in the minimum open position. This modification was installed
      safety-related function during certain postaccident conditions. The inspectors reviewed
to place the damper in its fail safe position after identifying that a loss of
      the following documentation during this inspection activity:
nonsafety-related instrument air would prevent the valve from performing its
      *       Condition Report CR-WF3-2003-00062
safety-related function during certain postaccident conditions. The inspectors reviewed
      *       EC-F00-0026, Post Fire Safe Shutdown Analysis
the following documentation during this inspection activity:
      *       Updated Final Safety Analysis Report, Section 9.4.3, Reactor Auxiliary Building
*
              Ventilation
Condition Report CR-WF3-2003-00062
b.   Findings
*
      No findings of significance were identified.
EC-F00-0026, Post Fire Safe Shutdown Analysis
*
Updated Final Safety Analysis Report, Section 9.4.3, Reactor Auxiliary Building
Ventilation
  b.
Findings
No findings of significance were identified.
Emergency Preparedness (EP)
Emergency Preparedness (EP)
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
1EP4
a.   Inspection Scope
Emergency Action Level and Emergency Plan Changes (71114.04)
      The inspector performed an in-office review of Revision 28 to the Waterford 3
  a.
      Emergency Plan, submitted January 15, 2003. Revision 28 changed organizational
Inspection Scope
      titles, updated facility and equipment information, clarified the revision process for the
The inspector performed an in-office review of Revision 28 to the Waterford 3
      emergency plan and emergency action levels, and made editorial corrections.
Emergency Plan, submitted January 15, 2003. Revision 28 changed organizational
      Revision 28 also implemented aspects of the removal of the postaccident sampling
titles, updated facility and equipment information, clarified the revision process for the
      system as approved in Technical Specification Amendment 172. The inspector
emergency plan and emergency action levels, and made editorial corrections.  
      compared Revision 28 with its previous revision and with the requirements of 10 CFR
Revision 28 also implemented aspects of the removal of the postaccident sampling
      50.54(q) to determine if the revision decreased the effectiveness of the emergency plan.
system as approved in Technical Specification Amendment 172. The inspector
b.   Findings
compared Revision 28 with its previous revision and with the requirements of 10 CFR
      No findings of significance were identified.
50.54(q) to determine if the revision decreased the effectiveness of the emergency plan.
  b.
Findings
No findings of significance were identified.


                                              -12-
-12-
1EP6 Drill Evaluation (71114.06)
1EP6
  a. Inspection Scope
Drill Evaluation (71114.06)
    The inspectors reviewed the drill scenario and observed activities in the simulated
  a.
    control room and the emergency operations facility. The drill scenario simulated
Inspection Scope
    equipment failures, a site evacuation, a loss of coolant accident, and the release of
The inspectors reviewed the drill scenario and observed activities in the simulated
    radioactive material offsite. In addition, the inspectors reviewed the drill critiques and
control room and the emergency operations facility. The drill scenario simulated
    the resolution of identified performance problems. The drill was conducted on
equipment failures, a site evacuation, a loss of coolant accident, and the release of
    March 13, 2003.
radioactive material offsite. In addition, the inspectors reviewed the drill critiques and
  b. Findings
the resolution of identified performance problems. The drill was conducted on
    No findings of significance were identified.
March 13, 2003.
4   OTHER ACTIVITIES (OA)
  b.
4OA1 Performance Indicator Verification (71151)
Findings
  .1 Initiating Events and Barrier Integrity Performance
No findings of significance were identified.
  a. Inspection Scope
4
    The inspectors reviewed data for initiating events and barrier integrity cornerstone
OTHER ACTIVITIES (OA)
    performance indicators from the fourth quarter of 2001 through the third quarter of 2002
4OA1 Performance Indicator Verification (71151)  
    for the following:
  .1
    *       Performance indicator data for unplanned power changes per 7,000 critical
Initiating Events and Barrier Integrity Performance
              hours
  a.
    *       Performance indicator data for scrams with loss of normal heat removal
Inspection Scope
    *       Performance indicator data for safety system unavailability/emergency ac power
The inspectors reviewed data for initiating events and barrier integrity cornerstone
  b. Findings
performance indicators from the fourth quarter of 2001 through the third quarter of 2002
    No findings of significance were identified.
for the following:
4OA2 Identification and Resolution of Problems (71152)
*
  a. Inspection Scope
Performance indicator data for unplanned power changes per 7,000 critical
    The inspectors reviewed the licensees corrective actions associated with the failure of
hours
    Main Steam Admission Valve MS-401B for the turbine-driven emergency feedwater
*
    pump. This valve failed to operate during surveillance testing on March 9, 2003. The
Performance indicator data for scrams with loss of normal heat removal
    inspectors reviewed Condition Report CR-WF3-2003-00616 to ensure the full extent of
*
Performance indicator data for safety system unavailability/emergency ac power
  b.
Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)  
  a.
Inspection Scope
The inspectors reviewed the licensees corrective actions associated with the failure of
Main Steam Admission Valve MS-401B for the turbine-driven emergency feedwater
pump. This valve failed to operate during surveillance testing on March 9, 2003. The
inspectors reviewed Condition Report CR-WF3-2003-00616 to ensure the full extent of


                                                -13-
-13-
    the issue was identified, appropriate evaluations were performed, and corrective actions
the issue was identified, appropriate evaluations were performed, and corrective actions
    were specified and prioritized. Additionally, the inspectors reviewed maintenance history
were specified and prioritized. Additionally, the inspectors reviewed maintenance history
    on the valve to ensure that maintenance activities were accomplished in accordance
on the valve to ensure that maintenance activities were accomplished in accordance
    with vendor recommendations and specifications.
with vendor recommendations and specifications.
b. Findings
  b.
    No findings of significance were identified.
Findings
No findings of significance were identified.
4OA3 Event Followup (71153)
4OA3 Event Followup (71153)
a. Inspection Scope
  a.
    On February 14, 2003, the plant experienced a main turbine trip and subsequent reactor
Inspection Scope
    power cutback while transferring Electrical Bus 3AB to an alternate power supply. On
On February 14, 2003, the plant experienced a main turbine trip and subsequent reactor
    February 15, 2003, the reactor was subsequently shut down after identifying insulation
power cutback while transferring Electrical Bus 3AB to an alternate power supply. On
    degradation affecting the main generator exciter armature. The inspectors assessed
February 15, 2003, the reactor was subsequently shut down after identifying insulation
    plant response to the transient conditions resulting from the turbine trip to verify safety
degradation affecting the main generator exciter armature. The inspectors assessed
    systems performed appropriately. The inspectors reviewed the licensees actions to
plant response to the transient conditions resulting from the turbine trip to verify safety
    identify and correct those degraded conditions that could impact plant restart.
systems performed appropriately. The inspectors reviewed the licensees actions to
b. Findings
identify and correct those degraded conditions that could impact plant restart.
    Introduction: A Green self-revealing finding was identified for the failure to maintain and
  b.
    operate main generator seal oil backup differential pressure regulating Valve SO-308 in
Findings
    accordance with vendor recommendations. This condition resulted in a turbine trip and
Introduction: A Green self-revealing finding was identified for the failure to maintain and
    subsequent reactor power cutback on February 14, 2003.
operate main generator seal oil backup differential pressure regulating Valve SO-308 in
    Description: On February 14, 2003, the licensee transferred Electrical Bus 3AB to an
accordance with vendor recommendations. This condition resulted in a turbine trip and
    alternate power supply. The electrical bus transfer resulted in the loss of one of the two
subsequent reactor power cutback on February 14, 2003.
    available air side seal oil pumps. During the bus transfer, a turbine trip occurred due to
Description: On February 14, 2003, the licensee transferred Electrical Bus 3AB to an
    low generator seal oil differential pressure. The licensees investigation revealed that
alternate power supply. The electrical bus transfer resulted in the loss of one of the two
    seal oil backup differential pressure regulating Valve SO-308 had operated slowly and
available air side seal oil pumps. During the bus transfer, a turbine trip occurred due to
    was set at an inappropriate pressure that ultimately resulted in the turbine trip. Vendor
low generator seal oil differential pressure. The licensees investigation revealed that
    recommendations consisted of setting the pressure regulator to a setpoint of 8 psid.
seal oil backup differential pressure regulating Valve SO-308 had operated slowly and
    The setpoint for the regulator was found to be set at approximately 3 psid, which was
was set at an inappropriate pressure that ultimately resulted in the turbine trip. Vendor
    below the turbine trip setpoint. The licensee also noted that the vendor recommended
recommendations consisted of setting the pressure regulator to a setpoint of 8 psid.  
    monthly cycling of Valve SO-308 to verify its proper operation was never implemented
The setpoint for the regulator was found to be set at approximately 3 psid, which was
    nor contained in a maintenance instruction.
below the turbine trip setpoint. The licensee also noted that the vendor recommended
    Analysis: The inspectors determined this finding was more than minor because it
monthly cycling of Valve SO-308 to verify its proper operation was never implemented
    caused a perturbation in plant stability resulting in a reactor power cutback. Although
nor contained in a maintenance instruction.
    the finding resulted in a plant transient, the inspectors determined that it did not
Analysis: The inspectors determined this finding was more than minor because it
    contribute to the likelihood of a primary or secondary system loss-of-coolant accident
caused a perturbation in plant stability resulting in a reactor power cutback. Although
    initiator, did not contribute to the loss of mitigation equipment functions, and did not
the finding resulted in a plant transient, the inspectors determined that it did not
    increase the likelihood of a fire or internal/external flood. Therefore, the failure to
contribute to the likelihood of a primary or secondary system loss-of-coolant accident
    maintain and operate seal oil backup differential pressure regulating Valve SO-308 in
initiator, did not contribute to the loss of mitigation equipment functions, and did not
increase the likelihood of a fire or internal/external flood. Therefore, the failure to
maintain and operate seal oil backup differential pressure regulating Valve SO-308 in


                                              -14-
-14-
    accordance with vendor recommendations was of very low safety significance (Green).
accordance with vendor recommendations was of very low safety significance (Green).  
    The licensee documented this issue in their corrective action process as Condition
The licensee documented this issue in their corrective action process as Condition
    Report CR-WF3-2003-0408.
Report CR-WF3-2003-0408.
    Enforcement: No violation of regulatory requirements occurred. The inspectors
Enforcement: No violation of regulatory requirements occurred. The inspectors
    determined that the finding did not represent a noncompliance because it occurred on
determined that the finding did not represent a noncompliance because it occurred on
    nonsafety-related secondary plant equipment.
nonsafety-related secondary plant equipment.  
4OA6 Meetings
4OA6 Meetings
    Exit Meeting Summary
Exit Meeting Summary
1. The reactor inspector presented the inspection results to Mr. Joseph Venable,
  1.
    Waterford Vice President, and other members of licensee management at the
The reactor inspector presented the inspection results to Mr. Joseph Venable,
    conclusion of the inspection on January 17, 2003.
Waterford Vice President, and other members of licensee management at the
2. The inspector presented the inspection results to Mr. J. Lewis, Emergency Planning
conclusion of the inspection on January 17, 2003.
    Manager, and other members of licensee management during a telephonic exit interview
  2.
    conducted on March 18, 2003. The licensee acknowledged the findings presented.
The inspector presented the inspection results to Mr. J. Lewis, Emergency Planning
3. The resident inspectors presented the inspection results to Mr. Joseph Venable,
Manager, and other members of licensee management during a telephonic exit interview
    Waterford Vice President, and other members of licensee management at the
conducted on March 18, 2003. The licensee acknowledged the findings presented.
    conclusion of the inspection on March 24, 2003. The licensee acknowledged the
  3.
    findings presented.
The resident inspectors presented the inspection results to Mr. Joseph Venable,
    The inspectors asked the licensee whether any materials examined during the
Waterford Vice President, and other members of licensee management at the
    inspection should be considered proprietary. No proprietary information was identified.
conclusion of the inspection on March 24, 2003. The licensee acknowledged the
findings presented.
The inspectors asked the licensee whether any materials examined during the
inspection should be considered proprietary. No proprietary information was identified.
4OA7 Licensee Identified Violations
4OA7 Licensee Identified Violations
    The following violation of very low safety significance (Green) was identified by the
The following violation of very low safety significance (Green) was identified by the
    licensee and is a violation of NRC requirements, which meets the criteria of Section VI
licensee and is a violation of NRC requirements, which meets the criteria of Section VI
    of the NRC Enforcement Policy, NUREG-1600, for being dispositioned a noncited
of the NRC Enforcement Policy, NUREG-1600, for being dispositioned a noncited
    violation.
violation.
    10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part, that
10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part, that
    Measures shall be established to assure that applicable regulatory requirements and
Measures shall be established to assure that applicable regulatory requirements and
    the design basis are correctly translated into specifications, drawings, procedures, and
the design basis are correctly translated into specifications, drawings, procedures, and
    instructions. Contrary to this, the licensee identified that Component Cooling Water
instructions. Contrary to this, the licensee identified that Component Cooling Water
    Trains A and B total flow rates, in an accident condition, exceeded the maximum
Trains A and B total flow rates, in an accident condition, exceeded the maximum
    analyzed flow rates. This condition resulted in reducing the efficiency of the dry cooling
analyzed flow rates. This condition resulted in reducing the efficiency of the dry cooling
    towers to remove heat under certain environmental conditions. This was identified in the
towers to remove heat under certain environmental conditions. This was identified in the
    licensees corrective action process as Condition Report CR-WF3-2003-0512. This
licensees corrective action process as Condition Report CR-WF3-2003-0512. This
    finding is of very low safety significance because the design control deficiency did not
finding is of very low safety significance because the design control deficiency did not
    result in loss-of-system function as described in Generic Letter 91-18.
result in loss-of-system function as described in Generic Letter 91-18.


                              SUPPLEMENTAL INFORMATION
SUPPLEMENTAL INFORMATION
                          PARTIAL LIST OF PERSONS CONTACTED
PARTIAL LIST OF PERSONS CONTACTED
Licensee
Licensee
S. S. Anders, Superintendent, Plant Security
S. S. Anders, Superintendent, Plant Security
Line 692: Line 849:
J. Venable, Vice President, Operations
J. Venable, Vice President, Operations
K. T. Walsh, Manager, Operations
K. T. Walsh, Manager, Operations
                        ITEMS OPENED, CLOSED, AND DISCUSSED
ITEMS OPENED, CLOSED, AND DISCUSSED
  Opened
Opened
  50-382/0304-01       URI     Design Control of SVS-101 and SVS-102 (Section 1R04.1)
50-382/0304-01
  Discussed
URI
  Finding               FIN     Failure to Implement Vendor Recommendations
Design Control of SVS-101 and SVS-102 (Section 1R04.1)
                                (Section 40A3)
Discussed
                                  DOCUMENTS REVIEWED
Finding
FIN
Failure to Implement Vendor Recommendations
(Section 40A3)
DOCUMENTS REVIEWED
Procedures
Procedures
Operating Procedure OP-003-026, Cable Vault and Switchgear HVAC, Revision 7
Operating Procedure OP-003-026, Cable Vault and Switchgear HVAC, Revision 7
Line 707: Line 868:
Test, Revision 10
Test, Revision 10


                                              -2-
-2-
Surveillance Procedure OP-903-107, Plant Protection System Channel _A_B_C_D Functional
Surveillance Procedure OP-903-107, Plant Protection System Channel _A_B_C_D Functional
Test, Revision 14
Test, Revision 14
Line 734: Line 895:
429807, 433429, 438626
429807, 433429, 438626


                                            -3-
-3-
Work Order Package
Work Order Package
50231536, 00023206, 50231499, 50088469, 50010906, 00019905, 00023866, and 00020353
50231536, 00023206, 50231499, 50088469, 50010906, 00019905, 00023866, and 00020353
Condition Reports
Condition Reports
CR-WF3-1996-0686           CR-WF3-1996-00870             CR-WF3-1998-00250
CR-WF3-1996-0686
CR-WF3-1998-0591           CR-WF3-1999-00701             CR-WF3-2000-0698
CR-WF3-1996-00870
CR-WF3-2000-00839           CR-WF3-2000-00845             CR-WF3-2000-00855
CR-WF3-1998-00250
CR-WF3-2001-00775           CR-WF3-2001-00858             CR-WF3-2001-00863
CR-WF3-1998-0591
CR-WF3-2001-00900           CR-WF3-2001-00917             CR-WF3-2001-01112
CR-WF3-1999-00701
CR-WF3-2001-01344           CR-WF3-2001-01346             CR-WF3-2001-01347
CR-WF3-2000-0698
CR-WF3-2002-00900           CR-WF3-2002-00358             CR-WF3-2002-0563
CR-WF3-2000-00839
CR-WF3-2002-01596           CR-WF3-2003-00051             CR-WF3-2003-00052
CR-WF3-2000-00845
CR-WF3-2003-00053           CR-WF3-2003-00056             CR-WF3-2003-00069
CR-WF3-2000-00855
CR-WF3-2001-00775
CR-WF3-2001-00858
CR-WF3-2001-00863
CR-WF3-2001-00900
CR-WF3-2001-00917
CR-WF3-2001-01112
CR-WF3-2001-01344
CR-WF3-2001-01346
CR-WF3-2001-01347
CR-WF3-2002-00900
CR-WF3-2002-00358
CR-WF3-2002-0563
CR-WF3-2002-01596
CR-WF3-2003-00051
CR-WF3-2003-00052
CR-WF3-2003-00053
CR-WF3-2003-00056
CR-WF3-2003-00069
Engineering Reports
Engineering Reports
NUMBER               DESCRIPTION                                           REVISION
NUMBER
                    Maintenance Rule Periodic (a)(1) Assessment           Cycle 11
DESCRIPTION
                    Maintenance Rule Periodic (a)(1) Assessment           Cycle 10
REVISION
Maintenance Rule Periodic (a)(1) Assessment
Cycle 11
Maintenance Rule Periodic (a)(1) Assessment
Cycle 10
Licensee Event Reports
Licensee Event Reports
NUMBER                             DESCRIPTION                             REVISION
NUMBER
01-001       Violation of TS 3.3.1 because a TS channel check                 0
DESCRIPTION
            was not performed as required by TS 4.3.1.1
REVISION
01-003       Reactor Protection System Trip caused by Turbine                 0
01-001
            Governor Valve Oscillation
Violation of TS 3.3.1 because a TS channel check
01-004       Failure to enter TS action statement due to inadequate           0
      0
            surveillance test procedure
was not performed as required by TS 4.3.1.1
01-003
Reactor Protection System Trip caused by Turbine
      0
Governor Valve Oscillation
01-004
Failure to enter TS action statement due to inadequate  
      0
surveillance test procedure
Procedures
Procedures
NUMBER                             DESCRIPTION                             REVISION
NUMBER
DC-121               Maintenance Rule                                         0
DESCRIPTION
REVISION
DC-121
Maintenance Rule
      0


                                            -4-
-4-
Miscellaneous Documents
Miscellaneous Documents
NUMBER                             DESCRIPTION                 REVISION
NUMBER
                    Entergy South Maintenance Rule Desktop         1
DESCRIPTION
                    Core Protection Calculators (CPCs) Top Ten   1/9/03
REVISION
                    Equipment Issues Plan
Entergy South Maintenance Rule Desktop
                    Expert Panel Meeting Minutes               8/13/98
      1
                    Expert Panel Meeting Minutes               11/07/01
Core Protection Calculators (CPCs) Top Ten  
                              LIST OF ACRONYMS USED
  1/9/03
CFR             Code of Federal Regulations
Equipment Issues Plan
FIN             finding
Expert Panel Meeting Minutes
NRC             U. S. Nuclear Regulatory Commission
  8/13/98
URI             unresolved item
Expert Panel Meeting Minutes
11/07/01
LIST OF ACRONYMS USED
CFR
Code of Federal Regulations
FIN
finding
NRC
U. S. Nuclear Regulatory Commission
URI
unresolved item
}}
}}

Latest revision as of 10:46, 16 January 2025

IR 05000382-03-004, on 12/29/2002-03/22/2003; Entergy Operations, Inc.; Waterford Steam Electric Station; Unit 3; Event Followup
ML031070497
Person / Time
Site: Waterford Entergy icon.png
Issue date: 04/17/2003
From: William Jones
NRC/RGN-IV/DRP/RPB-E
To: Venable J
Entergy Operations
References
IR-03-004
Download: ML031070497 (24)


See also: IR 05000382/2003004

Text

April 17, 2003

Joseph E. Venable

Vice President Operations

Waterford 3

Entergy Operations, Inc.

17265 River Road

Killona, Louisiana 70066-0751

SUBJECT: NRC INSPECTION REPORT 50-382/03-04

Dear Mr. Venable:

On March 22, 2003, the NRC completed an inspection at your Waterford Steam Electric

Station, Unit 3. The enclosed report documents the inspection findings, which were discussed

on March 24, 2003, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, one self-revealing finding was identified that was

evaluated under the risk significance determination process as having very low safety

significance (Green). Additionally, a licensee identified violation is listed in Section 4OA7 of this

report. If you contest this noncited violation, you should provide a response within 30 days of

the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington DC 20555-0001; and the NRC

Resident Inspector at the Waterford Steam Electric Station, Unit 3, facility.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

William B. Jones

Project Branch E

Division of Reactor Projects

Entergy Operations, Inc.

-2-

Docket: 50-382

License: NPF-38

Enclosure:

NRC Inspection Report

50-382/03-04

cc w/enclosure:

Executive Vice President and

Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, Mississippi 39286-1995

Vice President, Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, Mississippi 39286-1995

Wise, Carter, Child & Caraway

P.O. Box 651

Jackson, Mississippi 39205

General Manager, Plant Operations

Waterford 3 SES

Entergy Operations, Inc.

17265 River Road

Killona, Louisiana 70066-0751

Manager - Licensing Manager

Waterford 3 SES

Entergy Operations, Inc.

17265 River Road

Killona, Louisiana 70066-0751

Chairman

Louisiana Public Service Commission

P.O. Box 91154

Baton Rouge, Louisiana 70821-9154

Director, Nuclear Safety &

Regulatory Affairs

Waterford 3 SES

Entergy Operations, Inc.

17265 River Road

Killona, Louisiana 70066-0751

Entergy Operations, Inc.

-3-

Michael E. Henry, Administrator

and State Liaison Officer

Department of Environmental Quality

P.O. Box 82135

Baton Rouge, Louisiana 70884-2135

Parish President

St. Charles Parish

P.O. Box 302

Hahnville, Louisiana 70057

Winston & Strawn

1400 L Street, N.W.

Washington, D.C. 20005-3502

Technological Services

Branch Chief

FEMA Region VI

800 North Loop 288

Federal Regional Center

Denton, Texas 76201-3698

Entergy Operations, Inc.

-4-

Electronic distribution by RIV:

Regional Administrator (EWM)

DRP Director (ATH)

DRS Director (DDC)

Senior Resident Inspector (MCH)

Branch Chief, DRP/E (WBJ)

Senior Project Engineer, DRP/E (VGG)

Staff Chief, DRP/TSS (PHH)

RITS Coordinator (NBH)

Brian McDermott (BJM)

WAT Site Secretary (AHY)

W. A. Maier, RSLO (WAM)

Dale Thatcher (DFT)

ADAMS:  Yes

 No Initials: ______

 Publicly Available  Nonpublicly Available

 Sensitive

 Nonsensitive

R:\\_WAT\\2003\\WT2003-04RP-MCH.wpd

RIV:RI:DRP/E

SRI:DRP/E

C:DRS/EMB

C:DRS/PSB

C:DRP/E

GFLarkin

MCHay

CSMarschall

TWPruett

WBJones

T - VGGaddy

T - VGGaddy

/RA/

E - MPShannon /RA/

4/11/03

4/11/03

4/11/03

4/9/03

4/17/03

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-382

License:

NPF-38

Report:

50-382/03-04

Licensee:

Entergy Operations, Inc.

Facility:

Waterford Steam Electric Station, Unit 3

Location:

Hwy. 18

Killona, Louisiana

Dates:

December 29, 2002, through March 22, 2003

Inspectors:

M. C. Hay, Senior Resident Inspector

G. F. Larkin, Resident Inspector

J. M. Mateychick, Reactor Inspector

P. A. Goldberg, Senior Reactor Inspector

Paul J. Elkmann, Emergency Preparedness Inspector

Approved By:

W. B. Jones, Chief, Project Branch E

Attachment:

Supplemental Information

SUMMARY OF FINDINGS

Waterford Steam Electric Station, Unit 3

NRC Inspection Report 50-382/03-04

IR05000382/2003-04; Entergy Operations, Inc.; on 12/29/2002-03/22/2003; Waterford Steam

Electric Station; Unit 3; Event Followup

The report covered a 12-week period of inspection by resident inspectors, an emergency

preparedness inspector, and a reactor inspector. The inspection identified one Green finding.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not

apply may be Green or be assigned a severity level after NRC management review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspector Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. A self-revealing finding was identified for the failure to maintain and

operate main generator seal oil backup differential pressure regulating

Valve SO-308 in accordance with vendor recommendations. This condition

resulted in a turbine trip and subsequent reactor power cutback on

February 14, 2003.

This self-revealing finding is greater than minor because it resulted in a

perturbation in plant stability resulting in a reactor power cutback, similar to

example 4.b in Appendix E of Manual Chapter 0612. The finding is of very low

safety significance because, although it caused a plant transient, it did not

increase the likelihood of a primary or secondary system loss-of-coolant accident

initiator, did not contribute to the loss of mitigation equipment functions, and did

not increase the likelihood of a fire or internal/external flood (Section 4OA3).

B.

Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee, was

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensee's corrective action program. The violation and corrective

action tracking number is listed in Section 4OA7.

Report Details

Summary of Plant Status: The plant was operated at approximately 100 percent power

December 29, 2002, through February 14, 2003. Power was reduced to approximately

60 percent power February 14, 2003, following a turbine trip and subsequent reactor power

cutback. The reactor was shutdown February 15, 2003, to support main turbine generator

repairs. On February 19, 2003, reactor power was restored to 100 percent. Reactor power

was maintained at approximately 100 percent throughout the remainder of the inspection

period.

1

REACTOR SAFETY

Initiating Events, Mitigating Systems, Barrier Integrity (R)

1R01

Adverse Weather Protection (71111.01)

a.

Inspection Scope

On January 23, 2003, the inspectors performed a walkdown of components and

systems susceptible to freezing using Procedure OP-002-007, Freeze Protection and

Temperature Maintenance, Revision 10, to verify that the onset of cold weather would

not affect mitigating systems. This inspection included a review of deficiency tags and

condition reports associated with heat tracing and other cold weather protection

measures to determine their impact on the systems. Additionally, the inspectors

discussed adverse weather preparations with various licensee personnel.

b.

Findings

No findings of significance were identified.

1R04

Equipment Alignment (71111.04)

.1

Reactor Auxiliary Building Cable Vault and Switchgear Area Ventilation System

a.

Inspection Scope

The inspectors performed a complete equipment alignment inspection of the reactor

auxiliary building cable vault and switchgear area ventilation system. A review of select

maintenance work orders and corrective action documents was performed to assess the

material condition and performance of the switchgear area ventilation system. System

configuration was assessed using Operating Procedure OP-003-026, "Cable Vault and

Switchgear HVAC," Revision 7. A walkdown of accessible portions of the system was

performed to assess material condition, such as system leaks and housekeeping issues,

that could adversely affect system operability. The inspection also consisted of verifying

that the system was installed, maintained, and tested as described in the Updated Final

Safety Analysis Report and Technical Specifications.

b.

Findings

Introduction: The NRC identified that Switchgear Ventilation System Trains A and B

safety-related outside air intake Dampers SVS-101 and SVS-102, respectively, are

-2-

susceptible to a common mode failure vulnerability associated with a loss of

nonsafety-related instrument air. Pending determination of the findings safety

significance, this finding is identified as Unresolved Item (URI) 50-382/03-04-01.

Description: Switchgear Ventilation System Trains A and B outside air intake

Dampers SVS-101 and SVS-102, respectively, are safety-related, installed in series,

and pneumatically operated. A safety injection actuation signal automatically positions

these dampers to a minimum open position using instrument air. The inspectors noted

that a loss of instrument air, which is a nonsafety-related system, would introduce a

common mode failure for Dampers SVS-101 and SVS-102 preventing these valves from

performing their safety-related function during certain postaccident conditions. In

response to this concern, the licensee took immediate corrective actions and gagged, in

the minimum open position, Damper SVS-102. A review of design documentation by

the inspectors and the licensee identified that the basis for the valves being positioned

in the minimum open position following a safety injection actuation signal was not clearly

documented. The licensee developed, but had yet to implement, a special test to

assess the effects on the control room envelope and those areas surrounding the

control room due to Dampers SVS-101 and SVS-102 failing in the open position.

Analysis: Using the guidance in Appendix B of Inspection Manual Chapter 0612, this

issue potentially will screen more than minor. The barrier integrity objective, to provide

reasonable assurance that the physical design barriers to protect the control room

operators from radionuclide releases caused by accidents or events, was affected.

A Phase 1 screening was performed for the issue utilizing NRC Manual Chapter 0609,

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Attachment 1. The finding was assessed as potentially affecting the

radiological barrier function for the control room. The significance of this issue is

unresolved pending the results of a special test that will determine the pressure effects

on the control room envelope following failure of Dampers SVS-101 and SVS-102 to

maintain their minimum open safety position following a safety injection actuation signal.

Enforcement: 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in

part, that Measures shall be established to assure that applicable regulatory

requirements and the design basis are correctly translated into specifications, drawings,

procedures, and instructions. The failure to maintain design control of the switchgear

ventilation system resulting in the potential common mode failure of Dampers SVS-101

and SVS-102, due to loss of the nonsafety related instrument air system, is being

considered a violation of 10 CFR Part 50, Appendix B, Criterion III. Pending

determination of the findings safety significance, this finding is identified as

URI 50-382/03-04-01. The licensee documented this issue in their corrective action

process as Condition Report CR-WF3-2003-0062.

-3-

.2

High-Pressure Safety Injection System Train A

a.

Inspection Scope

On February 4, 2003, the inspectors performed a partial walkdown of the mechanical

and electrical components of a critical portion of High-Pressure Safety Injection System

Train A while the train was in a standby alignment. This walkdown was completed

during scheduled maintenance that rendered Train B inoperable. The inspectors

verified that the system was installed, maintained, and tested as described in the

Updated Final Safety Analysis Report and Technical Specifications.

b.

Findings

No findings of significance were identified.

.3

Shield Building Ventilation System

a.

Inspection Scope

On January 29, 2003, the inspectors performed a partial walkdown of the mechanical

and electrical components of a critical portion of Shield Building Ventilation System

Train A. This walkdown was completed during scheduled maintenance that rendered

Train B inoperable. The inspectors verified that the system was installed, maintained,

and tested as described in the Updated Final Safety Analysis Report and Technical

Specifications.

b.

Findings

No findings of significance were identified.

.4

Component Cooling Water Train A

a.

Inspection Scope

On March 13, 2003, the inspectors completed a partial equipment alignment inspection

of Component Cooling Water Train A. A review of select maintenance work orders and

corrective action documents was performed to assess the material condition and

performance of Component Cooling Water Train A. System configuration was assessed

using Operating Procedure OP-002-003, "Component Cooling Water," Revision 13. A

walkdown of accessible portions of the system was performed to assess material

condition, such as system leaks and housekeeping issues, that could adversely affect

system operability.

b.

Findings

No findings of significance were identified.

-4-

1R05

Fire Protection (71111.05)

The inspectors conducted six inspections to determine if the licensee had implemented

a fire protection program that adequately controlled combustibles and ignition sources

within the plant, effectively maintained fire detection and suppression capabilities, and

maintained passive fire protection features in good material condition.

The following areas were inspected:

Reactor auxiliary building +21-foot elevation on January 23, 2003

Control room envelop on February 4, 2003

Safety Injection Pump Area B on February 4, 2003

Switchgear Room B on February 4, 2003

Reactor auxiliary building +46-foot elevation on February 20, 2003

Reactor auxiliary building -4-foot and -35-foot elevations on February 28, 2003

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification (71111.11)

a.

Inspection Scope

On February 3, 2003, the inspectors observed licensed operator simulator training. The

simulator training evaluated the operator's ability to recognize, diagnose, and respond to

a small tube leak in Steam Generator 1, a reactor trip with failure of two control element

assemblies to insert, and the failure of High-Pressure Safety Injection Pump B to start

on a safety injection actuation signal. The inspectors observed and evaluated the

following areas:

Understanding and interpreting annunciator and alarm signals

Diagnosing events and conditions based on signals or readings

Understanding plant systems

Use and adherence of Technical Specifications

Crew communications including command and control

The crew's and evaluator's critiques

b.

Findings

No findings of significance were identified.

-5-

1R12

Maintenance Rule Implementation (71111.12)

.1

Routine Maintenance Rule Review

a.

Inspection Scope

During the inspection period, the inspectors reviewed licensee implementation of the

Maintenance Rule. The inspectors considered the characterization, safety significance,

performance criteria, and appropriateness of goals and corrective actions. The

inspectors assessed the licensees implementation of the Maintenance Rule to the

requirements outlined in 10 CFR 50.65 and Regulatory Guide 1.160, Monitoring the

Effectiveness of Maintenance at Nuclear Power Plants, Revision 2. The inspectors

reviewed the following systems that displayed performance problems:

Emergency Diesel Generating System Train A

Containment Cooling HVAC Trains A and B

b.

Findings

No findings of significance were identified.

.2

Periodic Evaluation Reviews

a.

Inspection Scope

The inspectors reviewed the Waterford 3 report documenting the performance of the

last Maintenance Rule periodic effectiveness assessment. This periodic evaluation

covered the period from November 2000 through April 2002.

The inspectors reviewed the program for monitoring risk-significant functions associated

with structures, systems, and components using reliability and unavailability. The

performance monitoring of nonrisk-significant functions using plant level criteria was

also reviewed.

The inspectors evaluated whether the report contained adequate assessment of the

performance of the Maintenance Rule Program as well as conformance with applicable

programmatic and regulatory requirements. To accomplish this, the inspectors verified

that the licensee appropriately and correctly addressed the following attributes in the

assessment reports:

The program treatment of nonrisk-significant structure, system, and component

functions monitored against plant level performance criteria

Program adjustments made in response to unbalanced reliability and availability

The application of industry operating experience

-6-

Performance review of Category (a)(1) systems

Evaluation of the bases for system category status change (e.g., (a)(1) to (a)(2)

or (a)(2) to (a)(1))

Effectiveness of performance and condition monitoring at component, train,

system, and plant levels

Review and adjustment of definitions of functional failures

The inspector also verified that the issuance of the two most recent assessments met

the regulatory timeliness requirements.

The inspectors reviewed procedures, condition reports, and Category (a)(1) recovery

plans associated with the above activities for the following systems: core protection

calculator, emergency diesel generator sequencer, feedwater, broad range gas

monitors, process radiation monitors, essential chillers (refrigeration), and shutdown

cooling.

b.

Findings

No findings of significance were identified.

.3

Identification and Resolution of Problems

a.

Inspection Scope

The inspectors evaluated the use of the corrective action system within the Maintenance

Rule Program for issues associated with risk-significant systems. The inspectors

examined a sample of corrective action documents associated with systems which were,

or had been, in Maintenance Rule Category (a)(1), including recovery plans for

improving the system performance. The inspectors performed this review to establish

that the corrective action program was entered at the appropriate threshold for the

purpose of:

Implementing the corrective action process when a performance criterion was

exceeded

Correcting performance-related issues or conditions identified during the periodic

evaluation

Correcting generic issues or conditions identified during programmatic

assessments, audits, or surveillances.

The inspectors identified an observation concerning the licensee's implementation of

appropriate corrective actions to maintain the performance of the core protection

calculator system. The core protection calculator was placed in Maintenance Rule

-7-

status Category (a)(1) from July 2000 to February 2001 and again in December 2001

until the time of this inspection due to both functional failures and unavailability.

The inspectors reviewed the licensees goals for monitoring the performance of the core

protection calculator for the Maintenance Rule. The inspectors noted that one

performance criteria for each channel to remain in Category (a)(2) consisted of

functional failures that resulted in a spurious channel trip being < 20 functional failures

per 18-month period per channel. The inspectors found that Channel D is not meeting

this goal. The inspectors review of system performance since July 1999 against this

goal indicated that prior to July 2000 there was another period when Channel D was not

meeting the goal. In addition, the inspectors found that Channels B and C also had

periods of not meeting this goal, sometimes concurrently with Channel D. The licensee

stated that since 1999 there were 13 instances where one channel was in trip and a

second channel was in bypass.

The inspectors reviewed Condition Reports CR-WF3-2000-0839 and -2001-1346 and

found that the licensee's corrective actions were focused on replacing failed electronic

components and improving the ventilation flow through the core protection calculator

cabinets to reduce the operating temperature of the electronic components. The

licensee intends to maintain the current core protection calculators system until

replacement during Refueling Outage 14 in the fall of 2006.

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a.

Inspection Scope

The inspectors reviewed risk assessments for planned or emergent maintenance

activities to determine if the licensee met the requirements of 10 CFR 50.65(a)(4) for

assessing and managing any increase in risk from these activities. Risk evaluations of

the following five occurrences were reviewed:

On January 23, 2003, Nitrogen Gas Valve NG-709 was declared inoperable and

required emergent repairs.

On February 5, 2003, Emergency Feedwater Pump B was declared inoperable

and required emergent repairs.

On February 6, 2003, troubleshooting activities were performed to isolate a

ground on the control element drive mechanism control system.

On February 9, 2003, Main Steam Admission Valve MS-401B to the

turbine-driven auxiliary feedwater pump was declared inoperable and required

emergent repairs.

-8-

On March 14, 2003, the Plant Protection System Channel B High Log Power Trip

Bypass Module was replaced.

b.

Findings

No findings of significance were identified.

1R14

Personnel Performance During Nonroutine Plant Evolutions (71111.14)

a.

Inspection Scope

For the nonroutine events described below, the inspectors reviewed operator logs, plant

computer data, and strip charts to determine what occurred, how the operators

responded, and whether the response was in accordance with plant procedures:

On February 14, 2003, the inspectors observed the site response to a turbine trip

followed by a reactor power cutback from 100 percent power. Reactor power

was reduced to approximately 60 percent with the steam bypass control system

available to mitigate the transient. On February 15, 2003, the inspectors

observed the operators perform a reactor shutdown following the identification of

insulation degradation that affected the main generator exciter.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed the technical adequacy of four operability evaluations to verify

that they were sufficient to justify continued operation of a system or component. The

inspectors considered that, although equipment was potentially degraded, the operability

evaluation provided adequate justification that the equipment could still meet its

Technical Specification, Updated Final Safety Analysis Report, and design-bases

requirements and that the potential risk increase contributed by the degraded equipment

was thoroughly evaluated. The following evaluations were reviewed:

Operability evaluation addressing missing nuts, washers, and a U-bolt affecting

the auxiliary component cooling water system Wet Cooling Tower A (Condition

Report CR-WF3-2003-00089)

Operability evaluation addressing broken reach rod linkage affecting operation of

Containment Spray Valve CS-117B (Condition Report CR-WF3-2003-00309)

-9-

Operability evaluation addressing total component cooling water flow in the

accident alignment exceeding design flow rates (Condition Report CR-WF3-2003-00512)

Operability evaluation addressing degraded seal water flow to Charging Pump B

(Condition Report CR-WF3-2003-00640)

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope

The inspectors performed a review of operator workarounds. This review evaluated the

cumulative affects of current operator workarounds to assess the overall impact

affecting the operators ability to respond in a correct and timely manner to plant

transients and accidents.

b.

Findings

No findings of significance were identified.

1R19

Postmaintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed postmaintenance tests to verify system operability and

functional capabilities. The inspectors considered whether testing met design and

licensing bases, Technical Specifications, and licensee procedural requirements. The

inspectors reviewed the testing results for the following six components:

Essential Chiller A following a low refrigerant pressure trip due to refrigerant

leakage through a damaged dehydrator gasket joint on December 12, 2002

Nitrogen Gas Valve NG-811 following repair work on valve internal parts on

February 20, 2003

Nitrogen Gas Valve NG-709 following valve stroke failure on February 23, 2003

Chilled Water Valve CHW-900 following valve actuator maintenance on

February 25, 2003

Main Steam Valve MS-401B following motor replacement on March 10, 2003

Plant Protection System Channel B High Log Power Trip Bypass Module

following replacement on March 14, 2003

-10-

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors observed or reviewed the following six surveillance tests to ensure the

systems were capable of performing their safety function and to assess their operational

readiness. Specifically, the inspectors considered whether the following surveillance

tests met Technical Specifications, the Updated Final Safety Analysis Report, and

licensee procedural requirements:

Surveillance Procedure OP-903-030, Safety Injection Pump Operability

Verification, Revision 13, was reviewed on January 24, 2003. This surveillance

tested the functional capability of Low-Pressure Safety Injection Pump A.

Surveillance Procedure OP-903-046, Emergency Feedwater Pump Operability

Check, Revision 15, performed on February 5, 2002. This surveillance tested

the functional capability of motor-driven Emergency Feedwater Pump B.

Surveillance Procedure OP-903-107, Plant Protection System Channel

_A_B_C_D Functional Test, Revision 14, was reviewed on February 19, 2003.

This surveillance tested the bypass, pretrip, and trip actuation capability of Plant

Protection System Channel A.

Surveillance Procedure STA-001-001, Containment Air Lock Seal Leakage

Test, Revision 4, was reviewed on February 20, 2003. This surveillance tested

the containment air lock pressure decay rate.

Surveillance Procedure OP-903-102, Safety Channel Nuclear Instrumentation

Functional Test, Revision 10, was reviewed on February 21, 2003. This

surveillance tested the functional capability of the Excore Nuclear Safety

Channels.

Surveillance Procedure OP-903-043, Shield Building Ventilation System

Operability Check, Revision 9, was reviewed on March 10, 2003. This

surveillance tested stroke times for critical valves required to change position

and verified adequate flow rates through the filter media.

b.

Findings

No findings of significance were identified.

-11-

1R23

Temporary Plant Modifications (71111.23)

a.

Inspection Scope

The inspectors reviewed a temporary plant modification of the switchgear ventilation

system to ensure that the modification did not adversely affect system operability or

design requirements specified in the Updated Final Safety Analysis Report and

Technical Specifications. The modification consisted of gagging switchgear ventilation

system Damper SVS-102 in the minimum open position. This modification was installed

to place the damper in its fail safe position after identifying that a loss of

nonsafety-related instrument air would prevent the valve from performing its

safety-related function during certain postaccident conditions. The inspectors reviewed

the following documentation during this inspection activity:

Condition Report CR-WF3-2003-00062

EC-F00-0026, Post Fire Safe Shutdown Analysis

Updated Final Safety Analysis Report, Section 9.4.3, Reactor Auxiliary Building

Ventilation

b.

Findings

No findings of significance were identified.

Emergency Preparedness (EP)

1EP4

Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

The inspector performed an in-office review of Revision 28 to the Waterford 3

Emergency Plan, submitted January 15, 2003. Revision 28 changed organizational

titles, updated facility and equipment information, clarified the revision process for the

emergency plan and emergency action levels, and made editorial corrections.

Revision 28 also implemented aspects of the removal of the postaccident sampling

system as approved in Technical Specification Amendment 172. The inspector

compared Revision 28 with its previous revision and with the requirements of 10 CFR 50.54(q) to determine if the revision decreased the effectiveness of the emergency plan.

b.

Findings

No findings of significance were identified.

-12-

1EP6

Drill Evaluation (71114.06)

a.

Inspection Scope

The inspectors reviewed the drill scenario and observed activities in the simulated

control room and the emergency operations facility. The drill scenario simulated

equipment failures, a site evacuation, a loss of coolant accident, and the release of

radioactive material offsite. In addition, the inspectors reviewed the drill critiques and

the resolution of identified performance problems. The drill was conducted on

March 13, 2003.

b.

Findings

No findings of significance were identified.

4

OTHER ACTIVITIES (OA)

4OA1 Performance Indicator Verification (71151)

.1

Initiating Events and Barrier Integrity Performance

a.

Inspection Scope

The inspectors reviewed data for initiating events and barrier integrity cornerstone

performance indicators from the fourth quarter of 2001 through the third quarter of 2002

for the following:

Performance indicator data for unplanned power changes per 7,000 critical

hours

Performance indicator data for scrams with loss of normal heat removal

Performance indicator data for safety system unavailability/emergency ac power

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

a.

Inspection Scope

The inspectors reviewed the licensees corrective actions associated with the failure of

Main Steam Admission Valve MS-401B for the turbine-driven emergency feedwater

pump. This valve failed to operate during surveillance testing on March 9, 2003. The

inspectors reviewed Condition Report CR-WF3-2003-00616 to ensure the full extent of

-13-

the issue was identified, appropriate evaluations were performed, and corrective actions

were specified and prioritized. Additionally, the inspectors reviewed maintenance history

on the valve to ensure that maintenance activities were accomplished in accordance

with vendor recommendations and specifications.

b.

Findings

No findings of significance were identified.

4OA3 Event Followup (71153)

a.

Inspection Scope

On February 14, 2003, the plant experienced a main turbine trip and subsequent reactor

power cutback while transferring Electrical Bus 3AB to an alternate power supply. On

February 15, 2003, the reactor was subsequently shut down after identifying insulation

degradation affecting the main generator exciter armature. The inspectors assessed

plant response to the transient conditions resulting from the turbine trip to verify safety

systems performed appropriately. The inspectors reviewed the licensees actions to

identify and correct those degraded conditions that could impact plant restart.

b.

Findings

Introduction: A Green self-revealing finding was identified for the failure to maintain and

operate main generator seal oil backup differential pressure regulating Valve SO-308 in

accordance with vendor recommendations. This condition resulted in a turbine trip and

subsequent reactor power cutback on February 14, 2003.

Description: On February 14, 2003, the licensee transferred Electrical Bus 3AB to an

alternate power supply. The electrical bus transfer resulted in the loss of one of the two

available air side seal oil pumps. During the bus transfer, a turbine trip occurred due to

low generator seal oil differential pressure. The licensees investigation revealed that

seal oil backup differential pressure regulating Valve SO-308 had operated slowly and

was set at an inappropriate pressure that ultimately resulted in the turbine trip. Vendor

recommendations consisted of setting the pressure regulator to a setpoint of 8 psid.

The setpoint for the regulator was found to be set at approximately 3 psid, which was

below the turbine trip setpoint. The licensee also noted that the vendor recommended

monthly cycling of Valve SO-308 to verify its proper operation was never implemented

nor contained in a maintenance instruction.

Analysis: The inspectors determined this finding was more than minor because it

caused a perturbation in plant stability resulting in a reactor power cutback. Although

the finding resulted in a plant transient, the inspectors determined that it did not

contribute to the likelihood of a primary or secondary system loss-of-coolant accident

initiator, did not contribute to the loss of mitigation equipment functions, and did not

increase the likelihood of a fire or internal/external flood. Therefore, the failure to

maintain and operate seal oil backup differential pressure regulating Valve SO-308 in

-14-

accordance with vendor recommendations was of very low safety significance (Green).

The licensee documented this issue in their corrective action process as Condition

Report CR-WF3-2003-0408.

Enforcement: No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because it occurred on

nonsafety-related secondary plant equipment.

4OA6 Meetings

Exit Meeting Summary

1.

The reactor inspector presented the inspection results to Mr. Joseph Venable,

Waterford Vice President, and other members of licensee management at the

conclusion of the inspection on January 17, 2003.

2.

The inspector presented the inspection results to Mr. J. Lewis, Emergency Planning

Manager, and other members of licensee management during a telephonic exit interview

conducted on March 18, 2003. The licensee acknowledged the findings presented.

3.

The resident inspectors presented the inspection results to Mr. Joseph Venable,

Waterford Vice President, and other members of licensee management at the

conclusion of the inspection on March 24, 2003. The licensee acknowledged the

findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements, which meets the criteria of Section VI

of the NRC Enforcement Policy, NUREG-1600, for being dispositioned a noncited

violation.

10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part, that

Measures shall be established to assure that applicable regulatory requirements and

the design basis are correctly translated into specifications, drawings, procedures, and

instructions. Contrary to this, the licensee identified that Component Cooling Water

Trains A and B total flow rates, in an accident condition, exceeded the maximum

analyzed flow rates. This condition resulted in reducing the efficiency of the dry cooling

towers to remove heat under certain environmental conditions. This was identified in the

licensees corrective action process as Condition Report CR-WF3-2003-0512. This

finding is of very low safety significance because the design control deficiency did not

result in loss-of-system function as described in Generic Letter 91-18.

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensee

S. S. Anders, Superintendent, Plant Security

J. R. Douet, General Manager, Plant Operations

C. Fugate, Assistant Manager, Operations

T. Gaudet, Director, Planning and Scheduling

B. Houston, Superintendent, Radiation Protection

C. Lambert, Director, Engineering

J. Lewis, Emergency Planning Manager

R. Murillo, Acting Manager, Licensing

R. Osborne, Manager, System Engineering

K. Peters, Director, Nuclear Safety Assurance/Emergency Preparedness

J. Laque, Manager, Maintenance

G. Scott, Engineer, Licensing

T. E. Tankersley, Manager, Training

J. Venable, Vice President, Operations

K. T. Walsh, Manager, Operations

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-382/0304-01

URI

Design Control of SVS-101 and SVS-102 (Section 1R04.1)

Discussed

Finding

FIN

Failure to Implement Vendor Recommendations

(Section 40A3)

DOCUMENTS REVIEWED

Procedures

Operating Procedure OP-003-026, Cable Vault and Switchgear HVAC, Revision 7

Surveillance Procedure OP-903-046, Emergency Feedwater Pump Operability Check,

Revision 15

Technical Procedure PE-004-024, "ACCW and CCW System Flow Balance," Revision 1

Surveillance Procedure OP-903-102, Safety Channel Nuclear Instrumentation Functional

Test, Revision 10

-2-

Surveillance Procedure OP-903-107, Plant Protection System Channel _A_B_C_D Functional

Test, Revision 14

Surveillance Procedure STA-001-001, Containment Air Lock Seal Leakage Test, Revision 4

Operations Procedure OP-903-063, Chilled Water Operability Verification, Revision 11

Corrective Action Documents

CR 2003-0302,2002-2068, 2002-2097, CR 2003-0512, CR 2002-2073, CR 2003-0656,

and CR 2003-0167

Other

Vendor Technical Manual 457000142, "Zurn Industries Mechanical Draft Cooling Towers,"

Revision 11

Calculation Number MN(Q) 9-52, "UHS Performance Based on Test Data," Revision 1

Calculation Number MN(Q) 9-2, "Component Cooling Water System," Revision 1

Calculation Number EC-M95-008, "Ultimate Heat Sink Design Basis," Revision 1

Information Notice 96-01, "Potential for High Post-Accident Closed-Cycle Cooling Water

Temperatures to Disable Equipment Important to Safety

W3-DBD-037, "Essential Chilled Water System Design Bases Document," Revision 1

Technical Procedure PE_004-026, "HVC-101 and HVC-102 Leak Test," Revision 6

Calculation Number NOSG-LPLK-90-01, "Control Room Habitability," Revision 0

W3-DBD-038, "Safety Related HVAC - Control Room Design Bases Document," Revision 1

Calculation Number EC-S96-011, "LOCA Offsite and Control Room Radiological Dose

Consequences," Revision 1

Calculation Number EC-S97-025, "Control Room Habitability Following Accidental Chlorine

Release," Revision 1

Maintenance Action Items

429807, 433429, 438626

-3-

Work Order Package

50231536, 00023206, 50231499, 50088469, 50010906, 00019905, 00023866, and 00020353

Condition Reports

CR-WF3-1996-0686

CR-WF3-1996-00870

CR-WF3-1998-00250

CR-WF3-1998-0591

CR-WF3-1999-00701

CR-WF3-2000-0698

CR-WF3-2000-00839

CR-WF3-2000-00845

CR-WF3-2000-00855

CR-WF3-2001-00775

CR-WF3-2001-00858

CR-WF3-2001-00863

CR-WF3-2001-00900

CR-WF3-2001-00917

CR-WF3-2001-01112

CR-WF3-2001-01344

CR-WF3-2001-01346

CR-WF3-2001-01347

CR-WF3-2002-00900

CR-WF3-2002-00358

CR-WF3-2002-0563

CR-WF3-2002-01596

CR-WF3-2003-00051

CR-WF3-2003-00052

CR-WF3-2003-00053

CR-WF3-2003-00056

CR-WF3-2003-00069

Engineering Reports

NUMBER

DESCRIPTION

REVISION

Maintenance Rule Periodic (a)(1) Assessment

Cycle 11

Maintenance Rule Periodic (a)(1) Assessment

Cycle 10

Licensee Event Reports

NUMBER

DESCRIPTION

REVISION

01-001

Violation of TS 3.3.1 because a TS channel check

0

was not performed as required by TS 4.3.1.1

01-003

Reactor Protection System Trip caused by Turbine

0

Governor Valve Oscillation

01-004

Failure to enter TS action statement due to inadequate

0

surveillance test procedure

Procedures

NUMBER

DESCRIPTION

REVISION

DC-121

Maintenance Rule

0

-4-

Miscellaneous Documents

NUMBER

DESCRIPTION

REVISION

Entergy South Maintenance Rule Desktop

1

Core Protection Calculators (CPCs) Top Ten

1/9/03

Equipment Issues Plan

Expert Panel Meeting Minutes

8/13/98

Expert Panel Meeting Minutes

11/07/01

LIST OF ACRONYMS USED

CFR

Code of Federal Regulations

FIN

finding

NRC

U. S. Nuclear Regulatory Commission

URI

unresolved item