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{{#Wiki_filter:February 13, 2008
{{#Wiki_filter:February 13, 2008  
Mr. James McCarthy
Site Vice President
FPL Energy Point Beach, LLC
6610 Nuclear Road
Mr. James McCarthy  
Two Rivers, WI 54241
Site Vice President  
SUBJECT:       POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED
FPL Energy Point Beach, LLC  
                INSPECTION REPORT 05000266/2007005 AND 05000301/2007005
6610 Nuclear Road  
Dear Mr. McCarthy:
Two Rivers, WI 54241  
On December 31, 2007, the U.S. Nuclear Regulatory Commission (NRC)
completed an integrated inspection at your Point Beach Nuclear Plant, Units 1 and 2.
SUBJECT:  
The enclosed inspection report documents the inspection results, which were discussed
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED  
on January 10, 2008, with you and members of your staff.
INSPECTION REPORT 05000266/2007005 AND 05000301/2007005
The inspection examined activities conducted under your license as they relate to safety and
Dear Mr. McCarthy:  
compliance with the Commissions rules and regulations, and with the conditions of your
On December 31, 2007, the U.S. Nuclear Regulatory Commission (NRC)  
license. The inspectors reviewed selected procedures and records, observed activities, and
completed an integrated inspection at your Point Beach Nuclear Plant, Units 1 and 2.
interviewed your personnel.
The enclosed inspection report documents the inspection results, which were discussed  
Based on the results of this inspection, seven NRC-identified and self-revealed findings of very
on January 10, 2008, with you and members of your staff.  
low safety significance (Green) were identified. Five of these findings were determined to
The inspection examined activities conducted under your license as they relate to safety and  
involve violations of NRC requirements. However, because of the very low safety significance
compliance with the Commissions rules and regulations, and with the conditions of your  
and because they are entered into your corrective action program, the NRC is treating these
license. The inspectors reviewed selected procedures and records, observed activities, and  
findings as Non-Cited Violations (NCVs), consistent with Section VI.A.1 of the NRC
interviewed your personnel.
Enforcement Policy. If you contest any NCV in this report, you should provide a response
Based on the results of this inspection, seven NRC-identified and self-revealed findings of very  
within 30 days of the date of this inspection report, with the basis for your denial, to the
low safety significance (Green) were identified. Five of these findings were determined to  
U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC
involve violations of NRC requirements. However, because of the very low safety significance  
20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory
and because they are entered into your corrective action program, the NRC is treating these  
Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the
findings as Non-Cited Violations (NCVs), consistent with Section VI.A.1 of the NRC  
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC
Enforcement Policy. If you contest any NCV in this report, you should provide a response  
20555-0001; and the Resident Inspector Office at the Point Beach Nuclear Plant.
within 30 days of the date of this inspection report, with the basis for your denial, to the  
U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC  
20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory  
Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the  
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC  
20555-0001; and the Resident Inspector Office at the Point Beach Nuclear Plant.  


J. McCarthy                                   -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
J. McCarthy  
enclosure, and your response (if any) will be available electronically for public inspection in
the NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's document system (ADAMS), accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                    Sincerely,
-2-  
                                                    /RA/
                                                    Michael A. Kunowski, Chief
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
                                                    Branch 5
enclosure, and your response (if any) will be available electronically for public inspection in  
                                                    Division of Reactor Projects
the NRC Public Document Room or from the Publicly Available Records System (PARS)  
Docket Nos. 50-266; 50-301
component of NRC's document system (ADAMS), accessible from the NRC Web site at  
License Nos. DPR-24; DPR-27
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
Enclosure:     Inspection Report 05000266/2007005; 05000301/2007005
Sincerely,
                w/Attachment: Supplemental Information
cc w/encl:     M. Nazar, Senior Vice President and Nuclear
/RA/  
                Chief Operating Officer
Michael A. Kunowski, Chief  
              J. Stall, Senior Vice President and
Branch 5  
                Chief Nuclear Officer
Division of Reactor Projects  
              R. Kundalkar, Vice President, Nuclear Technical Services
Docket Nos. 50-266; 50-301  
              Licensing Manager, Point Beach Nuclear Plant
License Nos. DPR-24; DPR-27  
              M. Ross, Managing Attorney
Enclosure:  
              A. Fernandez, Senior Attorney
Inspection Report 05000266/2007005; 05000301/2007005  
              K. Duveneck, Town Chairman
  w/Attachment: Supplemental Information  
                Town of Two Creeks
              Chairperson
cc w/encl:  
                Public Service Commission of Wisconsin
M. Nazar, Senior Vice President and Nuclear  
              J. Kitsembel, Electric Division
                Public Service Commission of Wisconsin
              State Liaison Officer
  Chief Operating Officer  
J. Stall, Senior Vice President and
  Chief Nuclear Officer  
R. Kundalkar, Vice President, Nuclear Technical Services  
Licensing Manager, Point Beach Nuclear Plant  
M. Ross, Managing Attorney  
A. Fernandez, Senior Attorney  
K. Duveneck, Town Chairman  
  Town of Two Creeks  
Chairperson  
  Public Service Commission of Wisconsin  
J. Kitsembel, Electric Division  
  Public Service Commission of Wisconsin  
State Liaison Officer  


J. McCarthy                                                               -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
J. McCarthy  
enclosure, and your response (if any) will be available electronically for public inspection in
the NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's document system (ADAMS), accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                                                      Sincerely,
-2-  
                                                                                      Michael A. Kunowski, Chief
                                                                                      Branch 5
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
                                                                                      Division of Reactor Projects
enclosure, and your response (if any) will be available electronically for public inspection in  
Docket Nos. 50-266; 50-301
the NRC Public Document Room or from the Publicly Available Records System (PARS)  
License Nos. DPR-24; DPR-27
component of NRC's document system (ADAMS), accessible from the NRC Web site at  
Enclosure:               Inspection Report 05000266/2007005; 05000301/2007005
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
                            w/Attachment: Supplemental Information
Sincerely,
cc w/encl:               M. Nazar, Senior Vice President and Nuclear
                            Chief Operating Officer
                          J. Stall, Senior Vice President and
Michael A. Kunowski, Chief  
                            Chief Nuclear Officer
Branch 5  
                          R. Kundalkar, Vice President, Nuclear Technical Services
Division of Reactor Projects  
                          Licensing Manager, Point Beach Nuclear Plant
Docket Nos. 50-266; 50-301  
                          M. Ross, Managing Attorney
License Nos. DPR-24; DPR-27  
                          A. Fernandez, Senior Attorney
Enclosure:  
                          K. Duveneck, Town Chairman
Inspection Report 05000266/2007005; 05000301/2007005  
                            Town of Two Creeks
  w/Attachment: Supplemental Information  
                          Chairperson
                            Public Service Commission of Wisconsin
cc w/encl:  
                          J. Kitsembel, Electric Division
M. Nazar, Senior Vice President and Nuclear  
                            Public Service Commission of Wisconsin
                          State Liaison Officer
DOCUMENT NAME: G:\POIN\Poin 2007 005.doc
  Chief Operating Officer  
  Publicly Available                         Non-Publicly Available                   Sensitive             Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE                 RIII                               RIII
J. Stall, Senior Vice President and
  NAME                   RKrsek*MAK for                     MKunowski
  DATE                   2/13/08                           2/13/08
                                                          OFFICIAL RECORD COPY
  Chief Nuclear Officer  
R. Kundalkar, Vice President, Nuclear Technical Services  
Licensing Manager, Point Beach Nuclear Plant  
M. Ross, Managing Attorney  
A. Fernandez, Senior Attorney  
K. Duveneck, Town Chairman  
  Town of Two Creeks  
Chairperson  
  Public Service Commission of Wisconsin  
J. Kitsembel, Electric Division  
  Public Service Commission of Wisconsin  
State Liaison Officer  
DOCUMENT NAME: G:\\POIN\\Poin 2007 005.doc  
  Publicly Available  
Non-Publicly Available  
Sensitive  
Non-Sensitive  
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy  
OFFICE  
RIII  
RIII  
   
NAME  
RKrsek*MAK for  
MKunowski  
   
DATE  
2/13/08  
2/13/08  
OFFICIAL RECORD COPY  


Letter to J. McCarthy from M. Kunowski dated February 13, 2008.
SUBJECT:       POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED
Letter to J. McCarthy from M. Kunowski dated February 13, 2008.  
              INSPECTION REPORT 05000266/2007005 AND 05000301/2007005
SUBJECT:  
DISTRIBUTION:
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED  
TEB
INSPECTION REPORT 05000266/2007005 AND 05000301/2007005
CFL
EMH1
DISTRIBUTION:  
LXR1
TEB  
RidsNrrDirsIrib
CFL  
MAS
EMH1  
KGO
LXR1  
JKH3
RidsNrrDirsIrib  
CAA1
MAS  
RGK
KGO  
LSL (electronic IRs only)
JKH3  
C. Pederson, DRP (hard copy - IRs only)
CAA1  
DRPIII
RGK  
DRSIII
LSL (electronic IRs only)  
PLB1
C. Pederson, DRP (hard copy - IRs only)  
TXN
DRPIII  
ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)
DRSIII  
PLB1  
TXN  
ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)  


          U.S. NUCLEAR REGULATORY COMMISSION
Enclosure
                          REGION III
U.S. NUCLEAR REGULATORY COMMISSION  
Docket Nos:         50-266; 50-301
REGION III  
License Nos:       DPR-24; DPR-27
Docket Nos:  
Report No:         05000266/2007005; 05000301/2007005
50-266; 50-301  
Licensee:           FPL Energy Point Beach, LLC
License Nos:  
Facility:           Point Beach Nuclear Plant, Units 1 and 2
DPR-24; DPR-27  
Location:           Two Rivers, Wisconsin
Report No:  
Dates:             October 1, 2007, through December 31, 2007
05000266/2007005; 05000301/2007005
Inspectors:         R. Krsek, Senior Resident Inspector
Licensee:  
                    R. Ruiz, Resident Inspector
FPL Energy Point Beach, LLC  
                    S. Burton, Senior Resident Inspector, Kewaunee
Facility:  
                    P. Higgins, Resident Inspector, Kewaunee
Point Beach Nuclear Plant, Units 1 and 2  
                    W. Slawinski, Senior Health Physicist
Location:  
                    C. Zoia, Operations Engineer
Two Rivers, Wisconsin  
                    N. Valos, Senior Operations Engineer
Dates:  
                    K. Walton, Operations Engineer
October 1, 2007, through December 31, 2007  
                    R. Winter, Reactor Engineer
Inspectors:  
                    M. Jones, Reactor Engineer
R. Krsek, Senior Resident Inspector  
Approved by:       Michael Kunowski, Chief
                    Branch 5
R. Ruiz, Resident Inspector  
                    Division of Reactor Projects
                                                                  Enclosure
S. Burton, Senior Resident Inspector, Kewaunee  
P. Higgins, Resident Inspector, Kewaunee  
W. Slawinski, Senior Health Physicist  
C. Zoia, Operations Engineer  
N. Valos, Senior Operations Engineer  
K. Walton, Operations Engineer  
R. Winter, Reactor Engineer
M. Jones, Reactor Engineer  
Approved by:  
Michael Kunowski, Chief  
Branch 5  
Division of Reactor Projects  


                                    SUMMARY OF FINDINGS
IR 05000266/2007005, 05000301/20070005; 10/01/2007-12/31/2007; Point Beach Nuclear
2
Plant, Units 1 & 2; Adverse Weather Protection; Operability Evaluations; Followup of Events;
Enclosure
Other Activities.
SUMMARY OF FINDINGS  
This report covers a three-month period of inspections by resident inspectors and regional
IR 05000266/2007005, 05000301/20070005; 10/01/2007-12/31/2007; Point Beach Nuclear  
specialists. Seven Green findings were identified. Five of the findings which were identified
Plant, Units 1 & 2; Adverse Weather Protection; Operability Evaluations; Followup of Events;  
had associated Non-Cited Violations (NCVs). The significance of most findings is indicated
Other Activities.
by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
This report covers a three-month period of inspections by resident inspectors and regional  
Significance Determination Process, (SDP). Findings for which the SDP does not apply
specialists. Seven Green findings were identified. Five of the findings which were identified  
may be Green or be assigned a severity level after NRC management review. The NRCs
had associated Non-Cited Violations (NCVs). The significance of most findings is indicated  
program for overseeing the safe operation of commercial nuclear power reactors is described
by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,  
in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
Significance Determination Process, (SDP). Findings for which the SDP does not apply  
A.     NRC-Identified and Self-Revealing Findings
may be Green or be assigned a severity level after NRC management review. The NRCs  
        Cornerstone: Initiating Events
program for overseeing the safe operation of commercial nuclear power reactors is described  
        *       Green. The inspectors identified a finding of very low safety significance with no
in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.  
                associated violation of regulatory requirements for the licensees failure to control
A.  
                loose materials in the protected area. Specifically, the inspectors identified
NRC-Identified and Self-Revealing Findings  
                materials that were classified as tornado hazards per station procedure PC 99
Cornerstone: Initiating Events  
                near the Unit 1 and Unit 2 main and auxiliary transformers and the switchyard
*  
                boundary. Once notified, the licensee entered the issue into its corrective action
Green. The inspectors identified a finding of very low safety significance with no  
                program and removed the materials. In addition, a procedure change request
associated violation of regulatory requirements for the licensees failure to control  
                was initiated to incorporate tornado hazard walkdowns into the abnormal
loose materials in the protected area. Specifically, the inspectors identified  
                operating procedure for severe weather response.
materials that were classified as tornado hazards per station procedure PC 99  
                The finding is more than minor because if left uncorrected, the loose items would
near the Unit 1 and Unit 2 main and auxiliary transformers and the switchyard  
                become a more significant safety concern. The finding is of very low safety
boundary. Once notified, the licensee entered the issue into its corrective action  
                significance (Green) because it did not contribute to both the likelihood of a
program and removed the materials. In addition, a procedure change request  
                reactor trip and the likelihood that mitigation equipment or functions will not be
was initiated to incorporate tornado hazard walkdowns into the abnormal  
                available. Additionally, the inspectors determined that the finding had a cross-
operating procedure for severe weather response.  
                cutting aspect in the area of problem identification and resolution in that the
The finding is more than minor because if left uncorrected, the loose items would  
                licensee failed to take appropriate corrective actions to address safety issues and
become a more significant safety concern. The finding is of very low safety  
                adverse trends in a timely manner, commensurate with their safety significance
significance (Green) because it did not contribute to both the likelihood of a  
                and complexity (P.1(d)). (Section 1R01.1)
reactor trip and the likelihood that mitigation equipment or functions will not be  
        Cornerstone: Mitigating Systems
available. Additionally, the inspectors determined that the finding had a cross-
        *       Green. A self-revealed finding with no associated violation of regulatory
cutting aspect in the area of problem identification and resolution in that the  
                requirements was identified for an inadequate operability evaluation performed
licensee failed to take appropriate corrective actions to address safety issues and  
                in June 2007 for service water pump P-32C. Specifically, the pump failed its
adverse trends in a timely manner, commensurate with their safety significance  
                inservice test (IST) on high vibrations after approximately six hours of operation,
and complexity (P.1(d)). (Section 1R01.1)  
                but the operability evaluation had concluded the pump vibrations would not reach
Cornerstone: Mitigating Systems  
                the out-of-service limit until after 120 hours of continuous operation. Contributing
*  
                to the unanticipated early failure was the use of non-conservative decision-
Green. A self-revealed finding with no associated violation of regulatory  
                making and the use of a non-conservative assumption in the pumps vibration
requirements was identified for an inadequate operability evaluation performed  
                prediction model. The licensee entered this issue into its corrective action
in June 2007 for service water pump P-32C. Specifically, the pump failed its  
                program and P-32C was subsequently repaired and returned to service.
inservice test (IST) on high vibrations after approximately six hours of operation,  
                                                    2                                      Enclosure
but the operability evaluation had concluded the pump vibrations would not reach  
the out-of-service limit until after 120 hours of continuous operation. Contributing  
to the unanticipated early failure was the use of non-conservative decision-
making and the use of a non-conservative assumption in the pumps vibration  
prediction model. The licensee entered this issue into its corrective action  
program and P-32C was subsequently repaired and returned to service.  


  The finding is more than minor because it could reasonably be viewed as a
  precursor to a significant event. The finding is of very low safety significance
3
  (Green) because there was no design deficiency, no actual loss of safety
Enclosure
  function, no single train loss of safety function for greater than the Technical
The finding is more than minor because it could reasonably be viewed as a  
  Specification (TS) allowed outage time, and no risk due to external events.
precursor to a significant event. The finding is of very low safety significance  
  Additionally, the inspectors determined that the finding had a cross-cutting aspect
(Green) because there was no design deficiency, no actual loss of safety  
  in the area of human performance. Specifically, the licensee failed to use
function, no single train loss of safety function for greater than the Technical  
  conservative assumptions in decision-making affecting operability of safety-
Specification (TS) allowed outage time, and no risk due to external events.
  related equipment (H.1(b)). (Section 1R15.1)
Additionally, the inspectors determined that the finding had a cross-cutting aspect  
* Green. The inspectors identified a finding of very low safety significance (Green)
in the area of human performance. Specifically, the licensee failed to use  
  and an associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,
conservative assumptions in decision-making affecting operability of safety-
  Instructions, Procedures, and Drawings, for the failure to adequately assess
related equipment (H.1(b)). (Section 1R15.1)  
  operability of the Unit 2 2P-29 turbine-driven auxiliary feedwater (TDAFW) pump.
*  
  The licensee failed to implement procedural requirements regarding the
Green. The inspectors identified a finding of very low safety significance (Green)  
  immediate assessment of operability on September 24 and September 27, 2007,
and an associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,  
  for the increased water ingress into the turbine outboard bearing housing for the
Instructions, Procedures, and Drawings, for the failure to adequately assess  
  pump following maintenance activities. The licensee took corrective actions,
operability of the Unit 2 2P-29 turbine-driven auxiliary feedwater (TDAFW) pump.
  which included performing an operability evaluation on November 1 when the
The licensee failed to implement procedural requirements regarding the  
  next scheduled test again revealed higher than normal levels of water in the
immediate assessment of operability on September 24 and September 27, 2007,  
  bearing oil. However, the inspectors continued to identify, in the subsequent
for the increased water ingress into the turbine outboard bearing housing for the  
  revisions to the operability determination, that the licensee failed to utilize all the
pump following maintenance activities. The licensee took corrective actions,  
  data available to assess pump operability. At the end of the inspection period,
which included performing an operability evaluation on November 1 when the  
  the licensee continued to evaluate the causes and corrective actions to address
next scheduled test again revealed higher than normal levels of water in the  
  this finding.
bearing oil. However, the inspectors continued to identify, in the subsequent  
  The finding is more than minor because, if left uncorrected, the failure to properly
revisions to the operability determination, that the licensee failed to utilize all the  
  assess operability would result in the TDAFW pump being degraded, and
data available to assess pump operability. At the end of the inspection period,  
  possibly inoperable for more than the allowed outage time in accordance with
the licensee continued to evaluate the causes and corrective actions to address  
  TSs with no action being taken. The finding is of very low safety significance
this finding.  
  (Green) because the inadequate operability determination did not result in
The finding is more than minor because, if left uncorrected, the failure to properly  
  exceeding the allowed outage time of TSs before action was taken. Additionally,
assess operability would result in the TDAFW pump being degraded, and  
  the inspectors determined that the finding had a cross-cutting aspect in the area
possibly inoperable for more than the allowed outage time in accordance with  
  of human performance. Specifically, the licensee failed to use conservative
TSs with no action being taken. The finding is of very low safety significance  
  assumptions in decision-making affecting operability of safety-related equipment
(Green) because the inadequate operability determination did not result in  
  (H.1(b)). (Section 1R15.2)
exceeding the allowed outage time of TSs before action was taken. Additionally,  
* Green. A self-revealed finding and an associated Non-Cited Violation of
the inspectors determined that the finding had a cross-cutting aspect in the area  
  10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,
of human performance. Specifically, the licensee failed to use conservative  
  were identified for the failure to have adequate procedures to allow operators to
assumptions in decision-making affecting operability of safety-related equipment  
  properly set the thermostat of the Unit 2 refueling water storage tank (RWST)
(H.1(b)). (Section 1R15.2)  
  heaters and to ensure the RWST was recirculated frequently enough for the
*  
  temperature indicator to accurately measure bulk temperature. On
Green. A self-revealed finding and an associated Non-Cited Violation of  
  September 18, 2007, the Unit 2 RWST was found to be at 105 °F. This
10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,  
  temperature exceeded the TS-maximum allowable limit of 100 °F (97 °F
were identified for the failure to have adequate procedures to allow operators to  
  parametric) and could not be restored to acceptable limits before the eight-hour
properly set the thermostat of the Unit 2 refueling water storage tank (RWST)  
  TS action statement expired. As a result, a shutdown of Unit 2 was commenced.
heaters and to ensure the RWST was recirculated frequently enough for the  
  At 20 percent power, a return to full power began after the RWST temperature
temperature indicator to accurately measure bulk temperature. On  
  was restored to within acceptable limits. It was later identified that the undesired
September 18, 2007, the Unit 2 RWST was found to be at 105 °F. This  
  heat-up was caused by the incorrect setting of the controlling thermostat for the
temperature exceeded the TS-maximum allowable limit of 100 °F (97 °F  
  RWST heaters.
parametric) and could not be restored to acceptable limits before the eight-hour  
                                      3                                        Enclosure
TS action statement expired. As a result, a shutdown of Unit 2 was commenced.
At 20 percent power, a return to full power began after the RWST temperature  
was restored to within acceptable limits. It was later identified that the undesired  
heat-up was caused by the incorrect setting of the controlling thermostat for the  
RWST heaters.  


  The finding is more than minor because it is associated with the procedure
  quality and human performance attributes of the Mitigating Systems Cornerstone
4
  and affected the cornerstone objective to ensure the availability, reliability, and
Enclosure
  capability of systems that respond to initiating events to prevent undesirable
The finding is more than minor because it is associated with the procedure  
  consequences (i.e., core damage). The finding is of very low safety significance
quality and human performance attributes of the Mitigating Systems Cornerstone  
  (Green) because the elevated temperature of the RWST and subsequent
and affected the cornerstone objective to ensure the availability, reliability, and  
  shutdown sequence did not contribute to both the likelihood of a reactor trip and
capability of systems that respond to initiating events to prevent undesirable  
  the likelihood that mitigation equipment or functions would not be available.
consequences (i.e., core damage). The finding is of very low safety significance  
  Additionally, the inspectors determined that the finding had a cross-cutting aspect
(Green) because the elevated temperature of the RWST and subsequent  
  in the area of human performance. Specifically, human error prevention
shutdown sequence did not contribute to both the likelihood of a reactor trip and  
  techniques were not utilized prior to and during the thermostat setting task and
the likelihood that mitigation equipment or functions would not be available.
  personnel proceeded in the face of uncertainty and unexpected circumstances
Additionally, the inspectors determined that the finding had a cross-cutting aspect  
  (H.4(a)). (Section 4OA3.1)
in the area of human performance. Specifically, human error prevention  
* Green. The inspectors identified a finding of very low safety significance and an
techniques were not utilized prior to and during the thermostat setting task and  
  associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,
personnel proceeded in the face of uncertainty and unexpected circumstances  
  Instructions, Procedures, and Drawings, for the licensees failure to conduct
(H.4(a)). (Section 4OA3.1)  
  adequate post-maintenance testing of the Unit 1 1P-29 turbine-driven auxiliary
*  
  feedwater (TDAFW) pump following a ten-year overhaul of the turbine in
Green. The inspectors identified a finding of very low safety significance and an  
  May 2007. Specifically, the ten-year overhaul maintenance included bearing
associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,  
  replacement, but the TDAFW pump was not run long enough during testing for
Instructions, Procedures, and Drawings, for the licensees failure to conduct  
  bearing temperature to stabilize. The appropriate post-maintenance test would
adequate post-maintenance testing of the Unit 1 1P-29 turbine-driven auxiliary  
  have detected that the bearing temperatures were rising and required evaluation
feedwater (TDAFW) pump following a ten-year overhaul of the turbine in  
  prior to declaring the TDAFW pump operable. The licensee entered the issue
May 2007. Specifically, the ten-year overhaul maintenance included bearing  
  into its corrective action program and took immediate corrective actions.
replacement, but the TDAFW pump was not run long enough during testing for  
  Additionally, the licensee initiated changes to the inadequate procedures.
bearing temperature to stabilize. The appropriate post-maintenance test would  
  The finding is more than minor because, if left uncorrected, the issue would have
have detected that the bearing temperatures were rising and required evaluation  
  become a more significant safety concern. The inspectors determined this
prior to declaring the TDAFW pump operable. The licensee entered the issue  
  finding was not a design qualification deficiency resulting in a loss of function per
into its corrective action program and took immediate corrective actions.
  NRC Generic Letter 91-18, did not represent an actual loss of safety function of a
Additionally, the licensee initiated changes to the inadequate procedures.  
  system or train of equipment, and was not potentially risk-significant due to a
  seismic, fire, flooding, or severe weather initiating event. Therefore, the finding is
The finding is more than minor because, if left uncorrected, the issue would have  
  considered to be of very low safety significance (Green). Additionally, the
become a more significant safety concern. The inspectors determined this  
  inspectors determined that the finding had a cross-cutting aspect in the area of
finding was not a design qualification deficiency resulting in a loss of function per  
  human performance. Specifically, the licensee failed to ensure that procedures
NRC Generic Letter 91-18, did not represent an actual loss of safety function of a  
  were adequate and accurate to assure nuclear safety (H.2(c)). (Section 4OA5.1)
system or train of equipment, and was not potentially risk-significant due to a  
* Green. The inspectors identified a finding of very low safety significance and an
seismic, fire, flooding, or severe weather initiating event. Therefore, the finding is  
  associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XVI,
considered to be of very low safety significance (Green). Additionally, the  
  Corrective Action, for the failure to implement prompt corrective actions for the
inspectors determined that the finding had a cross-cutting aspect in the area of  
  degraded oil conditions initially identified with the Unit 2 2P-29 turbine-driven
human performance. Specifically, the licensee failed to ensure that procedures  
  auxiliary feedwater (TDAFW) pump on September 24, 2007, following
were adequate and accurate to assure nuclear safety (H.2(c)). (Section 4OA5.1)  
  maintenance. Following an additional oil sample with favorable results, the
  licensee incorrectly concluded, due to confirmational biases, that the high water
*  
  content of the first oil sample was an expected condition. The licensee wrote a
Green. The inspectors identified a finding of very low safety significance and an  
  condition report, but it was closed with no actions taken. In November 2007, the
associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XVI,  
  licensee identified that a significant degraded oil condition existed with the pump.
Corrective Action, for the failure to implement prompt corrective actions for the  
  The licensee entered the issue into its corrective action program and took
degraded oil conditions initially identified with the Unit 2 2P-29 turbine-driven  
  immediate corrective actions, including rebuilding the pump turbine. The
auxiliary feedwater (TDAFW) pump on September 24, 2007, following  
                                      4                                      Enclosure
maintenance. Following an additional oil sample with favorable results, the  
licensee incorrectly concluded, due to confirmational biases, that the high water  
content of the first oil sample was an expected condition. The licensee wrote a  
condition report, but it was closed with no actions taken. In November 2007, the  
licensee identified that a significant degraded oil condition existed with the pump.
The licensee entered the issue into its corrective action program and took  
immediate corrective actions, including rebuilding the pump turbine. The  


          licensee continued to evaluate the causes and corrective actions to address this
          finding at the end of the inspection period.
5
          The finding is more than minor because it could reasonably be viewed as a
Enclosure
          precursor to a significant event. Specifically, the failure to correct the cause of
licensee continued to evaluate the causes and corrective actions to address this  
          the oil degradation in a timely manner in September 2007 could have resulted in
finding at the end of the inspection period.  
          the failure of the 2P-29 TDAFW pump. The finding is of very low safety
          significance (Green) because there was no design deficiency, no actual loss of
The finding is more than minor because it could reasonably be viewed as a  
          safety function, no single train loss of safety function for greater than the TS
precursor to a significant event. Specifically, the failure to correct the cause of  
          allowed outage time, and no risk due to external events. Additionally, the
the oil degradation in a timely manner in September 2007 could have resulted in  
          inspectors determined that the finding had a cross-cutting area aspect in the
the failure of the 2P-29 TDAFW pump. The finding is of very low safety  
          area of problem identification and resolution. Specifically, the licensee failed to
significance (Green) because there was no design deficiency, no actual loss of  
          thoroughly evaluate the problem with water ingress into the oil, such that a
safety function, no single train loss of safety function for greater than the TS  
          resolution addressed the cause and extent of condition (P.1(c)).
allowed outage time, and no risk due to external events. Additionally, the  
          (Section 4OA5.2.b.1)
inspectors determined that the finding had a cross-cutting area aspect in the  
  Cornerstone: Other
area of problem identification and resolution. Specifically, the licensee failed to  
  *     Green. The inspectors identified a finding of very low safety significance and
thoroughly evaluate the problem with water ingress into the oil, such that a  
          an associated Non-Cited Violation of 10 CFR 72.48(c)(1) for the licensees
resolution addressed the cause and extent of condition (P.1(c)).
          failure to obtain a Certificate of Compliance (CoC) amendment pursuant to
(Section 4OA5.2.b.1)  
          10 CFR 72.244, for changes made in the spent fuel storage cask operating
          procedures during the 2004 loading campaign as described in the Final Safety
Cornerstone: Other
          Analysis Report. The procedure changes constituted a change in the terms,
*  
          conditions, or specifications incorporated in the CoC. Although the procedures
Green. The inspectors identified a finding of very low safety significance and  
          were contained in the Final Safety Analysis Report, the licensee failed to identify
an associated Non-Cited Violation of 10 CFR 72.48(c)(1) for the licensees  
          that TS 1.2.17a, 32PT Dry Storage Canister (DSC) Vacuum Drying Duration
failure to obtain a Certificate of Compliance (CoC) amendment pursuant to  
          Limit, was also affected by the procedure change and required prior NRC
10 CFR 72.244, for changes made in the spent fuel storage cask operating  
          approval. The licensee implemented corrective actions, which included revising
procedures during the 2004 loading campaign as described in the Final Safety  
          the loading procedure to reflect the sequence described in the FSAR prior to the
Analysis Report. The procedure changes constituted a change in the terms,  
          next cask loading campaign.
conditions, or specifications incorporated in the CoC. Although the procedures  
          This finding is more than minor because it had the potential to impact the NRCs
were contained in the Final Safety Analysis Report, the licensee failed to identify  
          ability to perform its regulatory function, since the licensee failed to receive NRC
that TS 1.2.17a, 32PT Dry Storage Canister (DSC) Vacuum Drying Duration  
          approval for a change in this licensed activity. The inspectors determined that
Limit, was also affected by the procedure change and required prior NRC  
          the finding was not suitable for SDP evaluation because the noncompliance
approval. The licensee implemented corrective actions, which included revising  
          involved 10 CFR Part 72 dry fuel storage activities. Therefore, this finding was
the loading procedure to reflect the sequence described in the FSAR prior to the  
          reviewed by regional management and dispositioned using traditional
next cask loading campaign.  
          enforcement. The finding was determined to be of very low safety significance
          (Green). (Section 4OA5.5)
This finding is more than minor because it had the potential to impact the NRCs  
B. Licensee-Identified Violations
ability to perform its regulatory function, since the licensee failed to receive NRC  
  No violations of significance were identified.
approval for a change in this licensed activity. The inspectors determined that  
                                              5                                        Enclosure
the finding was not suitable for SDP evaluation because the noncompliance  
involved 10 CFR Part 72 dry fuel storage activities. Therefore, this finding was  
reviewed by regional management and dispositioned using traditional  
enforcement. The finding was determined to be of very low safety significance  
(Green). (Section 4OA5.5)  
B.  
Licensee-Identified Violations  
No violations of significance were identified.  


                                          REPORT DETAILS
Summary of Plant Status
6
Unit 1 was at 100 percent power throughout the inspection period with the exception of brief
Enclosure
reductions in power during routine auxiliary feedwater pump and secondary system valve
REPORT DETAILS  
testing.
Summary of Plant Status  
Unit 2 was at 100 percent power throughout the inspection period with the exception of brief
Unit 1 was at 100 percent power throughout the inspection period with the exception of brief  
reductions in power during routine auxiliary feedwater pump and secondary system valve
reductions in power during routine auxiliary feedwater pump and secondary system valve  
testing.
testing.  
1.       REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Unit 2 was at 100 percent power throughout the inspection period with the exception of brief  
1R01 Adverse Weather Protection (71111.01)
reductions in power during routine auxiliary feedwater pump and secondary system valve  
  .1     Readiness For Impending Adverse Weather Condition - High Wind Conditions
testing.  
    a.   Inspection Scope
        Because high winds were forecast in the vicinity of the facility for October 18, 2007, the
1.  
        inspectors reviewed the licensees overall preparations for the expected weather
REACTOR SAFETY  
        conditions. The inspectors walked down important outdoors areas within the protected
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
        area, in addition to the licensees emergency alternating current (AC) power systems,
1R01 Adverse Weather Protection (71111.01)  
        because safety-related functions could be affected by, or required as a result of, high
.1  
        winds or tornado-generated missiles. The inspectors focused on the licensees
Readiness For Impending Adverse Weather Condition - High Wind Conditions  
        procedures used to respond to specified adverse weather conditions and toured the
a.  
        plant grounds for loose debris, which could become missiles during a tornado or high
Inspection Scope  
        winds condition. The inspectors evaluated the licensees preparations against the sites
Because high winds were forecast in the vicinity of the facility for October 18, 2007, the  
        procedures and evaluated the adequacy of the staffs response. The inspectors also
inspectors reviewed the licensees overall preparations for the expected weather  
        verified that the licensee was identifying adverse weather issues at an appropriate
conditions. The inspectors walked down important outdoors areas within the protected  
        threshold and entering them into its corrective action program in accordance with station
area, in addition to the licensees emergency alternating current (AC) power systems,  
        procedures.
because safety-related functions could be affected by, or required as a result of, high  
        This inspection constituted one sample prior to the onset of an adverse weather.
winds or tornado-generated missiles. The inspectors focused on the licensees  
    b.   Findings
procedures used to respond to specified adverse weather conditions and toured the  
        Introduction: The inspectors identified a finding of very low safety significance (Green)
plant grounds for loose debris, which could become missiles during a tornado or high  
        for the licensees failure to control loose materials in the protected area. Specifically, the
winds condition. The inspectors evaluated the licensees preparations against the sites  
        inspectors identified materials that were classified as tornado hazards per licensee
procedures and evaluated the adequacy of the staffs response. The inspectors also  
        procedure PC 99 and were near the Unit 1 and Unit 2 main and auxiliary transformers
verified that the licensee was identifying adverse weather issues at an appropriate  
        and the switchyard boundary. No violation of regulatory requirements occurred.
threshold and entering them into its corrective action program in accordance with station  
        Description: On October 18, 2007, the inspectors conducted a walkdown of the risk
procedures.  
        significant portions of the main and auxiliary power system to assess the licensees
This inspection constituted one sample prior to the onset of an adverse weather.  
        preparations to preclude or minimize potential damage from high winds associated with
b.  
        severe storms or tornadoes. During the walkdown, the inspectors identified a significant
Findings  
        quantity of unsecured materials meeting the definition of tornado hazards provided in
Introduction: The inspectors identified a finding of very low safety significance (Green)  
                                                    6                                      Enclosure
for the licensees failure to control loose materials in the protected area. Specifically, the  
inspectors identified materials that were classified as tornado hazards per licensee  
procedure PC 99 and were near the Unit 1 and Unit 2 main and auxiliary transformers  
and the switchyard boundary. No violation of regulatory requirements occurred.  
Description: On October 18, 2007, the inspectors conducted a walkdown of the risk  
significant portions of the main and auxiliary power system to assess the licensees  
preparations to preclude or minimize potential damage from high winds associated with  
severe storms or tornadoes. During the walkdown, the inspectors identified a significant  
quantity of unsecured materials meeting the definition of tornado hazards provided in  


Point Beach procedure PC 99, Tornado Hazards Inspection Checklist, near the subject
transformers. The inspectors concluded that high winds or tornadoes combined with the
7
proximity of the transformers to the large quantity of unsecured materials increased the
Enclosure
potential to damage the transformers or related electrical equipment. The inspectors
Point Beach procedure PC 99, Tornado Hazards Inspection Checklist, near the subject  
informed the licensee of the concern and the licensee took immediate corrective action
transformers. The inspectors concluded that high winds or tornadoes combined with the  
to clean the areas identified by the inspectors and entered the issue into the corrective
proximity of the transformers to the large quantity of unsecured materials increased the  
action program as corrective action program document (CAP, condition report)
potential to damage the transformers or related electrical equipment. The inspectors  
CAP 01114731. The licensee also commenced a walkdown of outside areas within the
informed the licensee of the concern and the licensee took immediate corrective action  
protected area to address extent of condition. In addition, the licensee initiated a
to clean the areas identified by the inspectors and entered the issue into the corrective  
procedure change request to incorporate tornado hazard walkdowns into Abnormal
action program as corrective action program document (CAP, condition report)  
Operating Procedure (AOP) 13C, Severe Weather Conditions.
CAP 01114731. The licensee also commenced a walkdown of outside areas within the  
Analysis: The inspectors determined that the failure of licensee personnel to control
protected area to address extent of condition. In addition, the licensee initiated a  
material in the protected area near risk significant equipment is a performance
procedure change request to incorporate tornado hazard walkdowns into Abnormal  
deficiency. Using the guidance contained in Inspection Manual Chapter (IMC) 0612,
Operating Procedure (AOP) 13C, Severe Weather Conditions.  
Power Reactor Inspection Reports. Appendix B, Issue Disposition Screening, dated
Analysis: The inspectors determined that the failure of licensee personnel to control  
September 20, 2007, the inspectors determined that the finding is more than minor
material in the protected area near risk significant equipment is a performance  
because, if left uncorrected, the loose items in the vicinity of the main and auxiliary
deficiency. Using the guidance contained in Inspection Manual Chapter (IMC) 0612,  
transformers, and near the switchyard, would become a more significant safety concern.
Power Reactor Inspection Reports. Appendix B, Issue Disposition Screening, dated  
The inspectors determined that the finding warranted evaluation using the Significance
September 20, 2007, the inspectors determined that the finding is more than minor  
Determination Process (SDP) because the finding is associated with an increase in the
because, if left uncorrected, the loose items in the vicinity of the main and auxiliary  
likelihood of an initiating event.
transformers, and near the switchyard, would become a more significant safety concern.
The inspectors evaluated the finding using IMC 0609, Appendix A, Attachment 1,
The inspectors determined that the finding warranted evaluation using the Significance  
Significance Determination of Reactor Inspection Findings for At-Power Situations,
Determination Process (SDP) because the finding is associated with an increase in the  
dated January 10, 2008. Using the Phase 1 SDP worksheet for the Initiating Event
likelihood of an initiating event.
Cornerstone, transient initiator contributor, the inspectors determined that the finding did
The inspectors evaluated the finding using IMC 0609, Appendix A, Attachment 1,  
not contribute to the likelihood of a primary or secondary system loss of coolant accident
Significance Determination of Reactor Inspection Findings for At-Power Situations,  
initiator; the finding did not contribute to both the likelihood of a reactor trip and the
dated January 10, 2008. Using the Phase 1 SDP worksheet for the Initiating Event  
likelihood that mitigation equipment or functions will not be available; and the finding did
Cornerstone, transient initiator contributor, the inspectors determined that the finding did  
not increase the likelihood of a fire or internal or external flooding. Therefore, the finding
not contribute to the likelihood of a primary or secondary system loss of coolant accident  
is determined to be of very low safety significance (Green).
initiator; the finding did not contribute to both the likelihood of a reactor trip and the  
The inspectors performed a review of past corrective action program documents to
likelihood that mitigation equipment or functions will not be available; and the finding did  
assess the effectiveness of the licensees corrective actions to address similar issues.
not increase the likelihood of a fire or internal or external flooding. Therefore, the finding  
is determined to be of very low safety significance (Green).  
The inspectors performed a review of past corrective action program documents to  
assess the effectiveness of the licensees corrective actions to address similar issues.
During this review, inspectors noted that an NRC-identified finding, 05000266/000301-
During this review, inspectors noted that an NRC-identified finding, 05000266/000301-
2006004-01, was issued in July 2006 for a nearly identical issue related to the failure to
2006004-01, was issued in July 2006 for a nearly identical issue related to the failure to  
control loose material in the protected area. Procedure PC 99 was created as a
control loose material in the protected area. Procedure PC 99 was created as a  
corrective action for that finding. In addition, inspectors noted that between May and
corrective action for that finding. In addition, inspectors noted that between May and  
September 2007, there have been a number of CAPs written as a result of the
September 2007, there have been a number of CAPs written as a result of the  
identification of tornado hazards in the protected area during the use of procedure
identification of tornado hazards in the protected area during the use of procedure  
PC 99. Consequently, the inspectors determined that the finding had a cross-cutting
PC 99. Consequently, the inspectors determined that the finding had a cross-cutting  
aspect in the area of problem identification and resolution. Specifically, the licensee
aspect in the area of problem identification and resolution. Specifically, the licensee  
failed to take appropriate corrective actions to address safety issues and adverse trends
failed to take appropriate corrective actions to address safety issues and adverse trends  
in a timely manner, commensurate with their safety significance and complexity (P.1(d)).
in a timely manner, commensurate with their safety significance and complexity (P.1(d)).  
Enforcement: The failure to maintain the protected area free of tornado hazards was not
Enforcement: The failure to maintain the protected area free of tornado hazards was not  
an activity affecting quality subject to 10 CFR Part 50, Appendix B, nor was a procedure
an activity affecting quality subject to 10 CFR Part 50, Appendix B, nor was a procedure  
required by license conditions or TSs violated. Therefore, while a performance
required by license conditions or TSs violated. Therefore, while a performance  
deficiency existed, no violation of regulatory requirements occurred. This is considered
deficiency existed, no violation of regulatory requirements occurred. This is considered  
a finding of very low safety significance (FIN 05000266/2007005-01;
a finding of very low safety significance (FIN 05000266/2007005-01;  
                                            7                                        Enclosure


      05000301/2007005-01). The licensee included this finding in its corrective action
      program as CAP 01114731.
8
.2   Winter Seasonal Readiness Preparations
Enclosure
  a. Inspection Scope
05000301/2007005-01). The licensee included this finding in its corrective action  
      The inspectors conducted a review of the licensees preparations for winter conditions to
program as CAP 01114731.  
      verify that the plants design features and implementation of procedures were sufficient
.2  
      to protect mitigating systems from the effects of adverse weather. Documentation for
Winter Seasonal Readiness Preparations
      selected risk-significant systems was reviewed to ensure that these systems would
a.  
      remain functional when challenged by inclement weather. During the inspection, the
Inspection Scope  
      inspectors focused on plant specific design features and the licensees procedures used
The inspectors conducted a review of the licensees preparations for winter conditions to  
      to prepare for the onset of cold weather. Additionally, the inspectors reviewed licensee
verify that the plants design features and implementation of procedures were sufficient  
      corrective actions for areas in the plant which previously had cold weather issues. Cold
to protect mitigating systems from the effects of adverse weather. Documentation for  
      weather protection equipment, such as the façade freeze heat tracing and temporary
selected risk-significant systems was reviewed to ensure that these systems would  
      area heaters, were verified to be in operation when applicable. The inspectors also
remain functional when challenged by inclement weather. During the inspection, the  
      reviewed corrective action program items to verify that the licensee was identifying cold
inspectors focused on plant specific design features and the licensees procedures used  
      weather issues at an appropriate threshold and entering them into the corrective action
to prepare for the onset of cold weather. Additionally, the inspectors reviewed licensee  
      program in accordance with procedures. The inspectors reviews focused specifically on
corrective actions for areas in the plant which previously had cold weather issues. Cold  
      the following plant systems due to their risk significance or susceptibility to cold weather
weather protection equipment, such as the façade freeze heat tracing and temporary  
      issues: main steam system and instrumentation, including the atmospheric steam
area heaters, were verified to be in operation when applicable. The inspectors also  
      dumps and the main steam isolation valve; emergency core cooling system, including
reviewed corrective action program items to verify that the licensee was identifying cold  
      the refueling water storage tank and associated piping; and the façade freeze system.
weather issues at an appropriate threshold and entering them into the corrective action  
      This inspection constituted one winter seasonal system readiness sample.
program in accordance with procedures. The inspectors reviews focused specifically on  
  b. Findings
the following plant systems due to their risk significance or susceptibility to cold weather  
      No findings of significance were identified.
issues: main steam system and instrumentation, including the atmospheric steam  
1R04 Equipment Alignment (71111.04)
dumps and the main steam isolation valve; emergency core cooling system, including  
.1   Quarterly Partial System Walkdowns
the refueling water storage tank and associated piping; and the façade freeze system.  
  a. Inspection Scope
This inspection constituted one winter seasonal system readiness sample.  
      The inspectors performed partial walkdowns of accessible portions of risk-significant
b.  
      systems to determine the operability of these systems. The inspectors utilized system
Findings  
      valve lineup and electrical breaker checklists, tank level books, plant drawings, and
No findings of significance were identified.  
      selected operating procedures to determine whether the systems were correctly aligned
1R04 Equipment Alignment (71111.04)  
      to perform the intended design functions. The inspectors also examined the material
.1  
      condition of the components and observed operating equipment parameters to
Quarterly Partial System Walkdowns  
      determine whether deficiencies existed. The inspectors reviewed completed work
a.  
      orders (WOs) and calibration records associated with the systems for issues that could
Inspection Scope  
      affect component or train functions. The inspectors used the information in the
The inspectors performed partial walkdowns of accessible portions of risk-significant  
      appropriate sections of the Final Safety Analysis Report (FSAR) to determine the
systems to determine the operability of these systems. The inspectors utilized system  
      functional requirements of the system.
valve lineup and electrical breaker checklists, tank level books, plant drawings, and  
      Partial system walkdowns of the following systems constituted two inspection procedure
selected operating procedures to determine whether the systems were correctly aligned  
      samples:
to perform the intended design functions. The inspectors also examined the material  
                                                8                                        Enclosure
condition of the components and observed operating equipment parameters to  
determine whether deficiencies existed. The inspectors reviewed completed work  
orders (WOs) and calibration records associated with the systems for issues that could  
affect component or train functions. The inspectors used the information in the  
appropriate sections of the Final Safety Analysis Report (FSAR) to determine the  
functional requirements of the system.  
Partial system walkdowns of the following systems constituted two inspection procedure  
samples:  


      *       Emergency diesel generator (EDG) G01 aligned to busses 1A05 and 2A05 while
              EDG G02 was out-of-service the week of October 22, 2007; and
9
      *       EDG G02 aligned to busses 1A05 and 2A05 while EDG G01 was out-of-service
Enclosure
              the week of November 19, 2007.
*  
  b. Findings
Emergency diesel generator (EDG) G01 aligned to busses 1A05 and 2A05 while  
      No findings of significance were identified.
EDG G02 was out-of-service the week of October 22, 2007; and  
.2   Semi-Annual Complete System Walkdown
*  
  a. Inspection Scope
EDG G02 aligned to busses 1A05 and 2A05 while EDG G01 was out-of-service  
      In November 2007, the inspectors performed a complete system alignment inspection of
the week of November 19, 2007.  
      the auxiliary feedwater (AFW) system for Units 1 and 2 to verify the functional capability
b.  
      of the system. This system was selected because it was considered both safety-
Findings  
      significant and risk-significant in the licensees probabilistic risk assessment. The
No findings of significance were identified.  
      inspectors walked down the system to review mechanical and electrical equipment line-
.2  
      ups, electrical power availability, system pressure and temperature indications,
Semi-Annual Complete System Walkdown  
      component labeling, component lubrication, component and equipment cooling, hangers
a.  
      and supports, operability of support systems, and to ensure that ancillary equipment or
Inspection Scope  
      debris did not interfere with equipment operation. A review of past and outstanding WOs
In November 2007, the inspectors performed a complete system alignment inspection of  
      was performed to determine whether any deficiencies significantly affected system
the auxiliary feedwater (AFW) system for Units 1 and 2 to verify the functional capability  
      function. In addition, the inspectors reviewed the CAP database to ensure that system
of the system. This system was selected because it was considered both safety-
      equipment alignment problems were being identified and appropriately resolved. The
significant and risk-significant in the licensees probabilistic risk assessment. The  
      documents used for the walkdown and issue review are listed in the attached List of
inspectors walked down the system to review mechanical and electrical equipment line-
      Documents Reviewed.
ups, electrical power availability, system pressure and temperature indications,  
      These activities constituted one complete system walkdown inspection procedure
component labeling, component lubrication, component and equipment cooling, hangers  
      sample.
and supports, operability of support systems, and to ensure that ancillary equipment or  
  b. Findings
debris did not interfere with equipment operation. A review of past and outstanding WOs  
      No findings of significance were identified.
was performed to determine whether any deficiencies significantly affected system  
1R05 Fire Protection (71111.05)
function. In addition, the inspectors reviewed the CAP database to ensure that system  
.1   Routine Resident Inspector Tours (71111.05Q)
equipment alignment problems were being identified and appropriately resolved. The  
  a. Inspection Scope
documents used for the walkdown and issue review are listed in the attached List of  
      The inspectors conducted fire protection walkdowns, which focused on the following
Documents Reviewed.  
      attributes: the availability, accessibility, and condition of fire fighting equipment; the
These activities constituted one complete system walkdown inspection procedure  
      control of transient combustibles and ignition sources; and the condition and status of
sample.  
      installed fire barriers. The inspectors selected fire areas for inspection based on the
b.  
      areas overall fire risk contribution, as documented in the Individual Plant Examination of
Findings  
      External Events, or the potential of a fire to impact equipment that could initiate a plant
No findings of significance were identified.  
      transient.
1R05 Fire Protection (71111.05)  
      In addition, the inspectors assessed these additional fire protection attributes during
.1  
      walkdowns: fire hoses and extinguishers were in the designated locations and available
Routine Resident Inspector Tours (71111.05Q)  
                                                  9                                      Enclosure
a.  
Inspection Scope  
The inspectors conducted fire protection walkdowns, which focused on the following  
attributes: the availability, accessibility, and condition of fire fighting equipment; the  
control of transient combustibles and ignition sources; and the condition and status of  
installed fire barriers. The inspectors selected fire areas for inspection based on the  
areas overall fire risk contribution, as documented in the Individual Plant Examination of  
External Events, or the potential of a fire to impact equipment that could initiate a plant  
transient.  
In addition, the inspectors assessed these additional fire protection attributes during  
walkdowns: fire hoses and extinguishers were in the designated locations and available  


      for immediate use; unobstructed fire detectors and sprinklers; transient material loading
      within the analyzed limits; and fire doors, dampers, and penetration seals in satisfactory
10
      condition. The inspectors also determined whether minor issues identified during the
Enclosure
      inspection were entered into the licensees corrective action program.
for immediate use; unobstructed fire detectors and sprinklers; transient material loading  
      The walkdown of the following selected fire zones constituted three inspection procedure
within the analyzed limits; and fire doors, dampers, and penetration seals in satisfactory  
      samples:
condition. The inspectors also determined whether minor issues identified during the  
      *       Unit 2 TDAF Room
inspection were entered into the licensees corrective action program.  
      *       EDG G01 Room
The walkdown of the following selected fire zones constituted three inspection procedure  
      *       EDG G02 Room
samples:  
  b. Findings
*  
      No findings of significance were identified.
Unit 2 TDAF Room  
.2   Annual Fire Protection Drill Observation (71111.05A)
*  
  a. Inspection Scope
EDG G01 Room  
      During this quarter, the inspectors observed two fire brigade activation drills: an
*  
      October 9, 2007, drill scenario that simulated a fire in the Unit 2 2P-2C charging pump
EDG G02 Room  
      room and a November 26 drill scenario that simulated a fire in the unit common cable
      spreading room. The combined drill observations were used to determine the readiness
b.  
      of the plant fire brigade to fight fires. The inspectors verified that the licensee staff
Findings  
      identified deficiencies, openly discussed them in a self-critical manner at the drill
No findings of significance were identified.  
      debriefs, and took appropriate corrective actions. Specific attributes evaluated were:
.2  
      (1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper
Annual Fire Protection Drill Observation (71111.05A)  
      use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;
a.  
      (4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade
Inspection Scope  
      leader communications, command, and control; (6) search for victims and propagation of
During this quarter, the inspectors observed two fire brigade activation drills: an  
      the fire into other plant areas; (7) smoke removal operations; (8) utilization of pre-
October 9, 2007, drill scenario that simulated a fire in the Unit 2 2P-2C charging pump  
      planned strategies; (9) adherence to the pre-planned drill scenario; and (10) drill
room and a November 26 drill scenario that simulated a fire in the unit common cable  
      objectives.
spreading room. The combined drill observations were used to determine the readiness  
      These activities constituted one annual fire protection inspection sample.
of the plant fire brigade to fight fires. The inspectors verified that the licensee staff  
  b. Findings
identified deficiencies, openly discussed them in a self-critical manner at the drill  
      No findings of significance were identified.
debriefs, and took appropriate corrective actions. Specific attributes evaluated were:
1R07 Heat Sink Performance (71111.07)
(1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper  
  a. Inspection Scope
use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;  
      The inspectors reviewed the licensees testing of the EDG G01 and G02 heat
(4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade  
      exchangers one month following their replacement to verify that potential deficiencies
leader communications, command, and control; (6) search for victims and propagation of  
      did not affect the licensees ability to detect degraded performance, and to identify any
the fire into other plant areas; (7) smoke removal operations; (8) utilization of pre-
      common cause issues that had the potential to increase risk, and to ensure that the
planned strategies; (9) adherence to the pre-planned drill scenario; and (10) drill  
      licensee was adequately addressing problems that could result in initiating events that
objectives.  
      would cause an increase in risk. The inspectors also verified that the new heat
These activities constituted one annual fire protection inspection sample.  
                                                  10                                      Enclosure
b.  
Findings  
No findings of significance were identified.  
1R07 Heat Sink Performance (71111.07)  
a.  
Inspection Scope  
The inspectors reviewed the licensees testing of the EDG G01 and G02 heat  
exchangers one month following their replacement to verify that potential deficiencies  
did not affect the licensees ability to detect degraded performance, and to identify any  
common cause issues that had the potential to increase risk, and to ensure that the  
licensee was adequately addressing problems that could result in initiating events that  
would cause an increase in risk. The inspectors also verified that the new heat  


      exchangers were less susceptible to lake grass fouling, than the original heat
      exchangers. The inspectors reviewed the licensees observations as compared against
11
      acceptance criteria, the correlation of scheduled testing and the frequency of testing,
Enclosure
      and the impact of instrument inaccuracies on test results. Inspectors also verified that
exchangers were less susceptible to lake grass fouling, than the original heat  
      test acceptance criteria considered differences between test conditions, design
exchangers. The inspectors reviewed the licensees observations as compared against  
      conditions, and testing criteria.
acceptance criteria, the correlation of scheduled testing and the frequency of testing,  
      This inspection constituted one inspection procedure sample.
and the impact of instrument inaccuracies on test results. Inspectors also verified that  
  b. Findings
test acceptance criteria considered differences between test conditions, design  
      No findings of significance were identified.
conditions, and testing criteria.  
1R11 Licensed Operator Requalification (71111.11)
This inspection constituted one inspection procedure sample.  
.1   Resident Inspector Quarterly Review
b.  
  a. Inspection Scope
Findings  
      In November 2007, the inspectors observed a crew of licensed operators in the plants
No findings of significance were identified.  
      simulator during licensed operator training to verify that operator performance was
1R11 Licensed Operator Requalification (71111.11)  
      adequate, evaluators were identifying and documenting crew performance problems,
.1  
      and training was being conducted in accordance with licensee procedures. The
Resident Inspector Quarterly Review
      inspectors evaluated the following areas:
a.  
      *       licensed operator performance;
Inspection Scope  
      *       crews clarity and formality of communications;
In November 2007, the inspectors observed a crew of licensed operators in the plants  
      *       ability to take timely actions in the conservative direction;
simulator during licensed operator training to verify that operator performance was  
      *       prioritization, interpretation, and verification of annunciator alarms;
adequate, evaluators were identifying and documenting crew performance problems,  
      *       correct use and implementation of abnormal and emergency procedures;
and training was being conducted in accordance with licensee procedures. The  
      *       control board manipulations;
inspectors evaluated the following areas:  
      *       oversight and direction from supervisors; and
*  
      *       ability to identify and implement appropriate TS actions and Emergency Plan
licensed operator performance;  
              actions and notifications.
*  
      The crews performance in these areas was compared to pre-established operator action
crews clarity and formality of communications;  
      expectations and successful critical task completion requirements.
*  
      This inspection constituted one quarterly licensed operator requalification program
ability to take timely actions in the conservative direction;  
      sample.
*  
  b. Findings
prioritization, interpretation, and verification of annunciator alarms;  
      No findings of significance were identified.
*  
.2   Facility Operating History
correct use and implementation of abnormal and emergency procedures;  
  a. Inspection Scope
*  
      The inspectors reviewed the plants operating history from September 2005 through
control board manipulations;  
      October 2007 to identify operating experience that was expected to be addressed by the
*  
                                                  11                                  Enclosure
oversight and direction from supervisors; and  
*  
ability to identify and implement appropriate TS actions and Emergency Plan  
actions and notifications.  
The crews performance in these areas was compared to pre-established operator action  
expectations and successful critical task completion requirements.  
This inspection constituted one quarterly licensed operator requalification program  
sample.  
b.  
Findings  
No findings of significance were identified.  
.2  
Facility Operating History  
a.  
Inspection Scope  
The inspectors reviewed the plants operating history from September 2005 through  
October 2007 to identify operating experience that was expected to be addressed by the  


      Licensed Operator Requalification Training (LORT) program. It was then verified that
      the identified operating experience had been addressed by the facility licensee in
12
      accordance with the stations approved Systems Approach to Training (SAT) program to
Enclosure
      satisfy the requirements of 10 CFR 55.59(c), Requalification program requirements.
Licensed Operator Requalification Training (LORT) program. It was then verified that  
  b. Findings
the identified operating experience had been addressed by the facility licensee in  
      No findings of significance were identified.
accordance with the stations approved Systems Approach to Training (SAT) program to  
.3   Licensee Requalification Examinations
satisfy the requirements of 10 CFR 55.59(c), Requalification program requirements.  
  a. Inspection Scope
b. Findings  
      The inspectors performed a biennial inspection of the licensees LORT test/examination
No findings of significance were identified.  
      program for compliance with the stations SAT program that would satisfy the
.3  
      requirements of 10 CFR 55.59(c)(4), Evaluation. The inspectors reviewed the 2006
Licensee Requalification Examinations  
      biennial written requalification examinations and 2007 annual operating test material to
a.  
      evaluate general quality, construction, and difficulty level. The written examinations
Inspection Scope  
      reviewed consisted of four written examinations, each containing 30 questions. The
The inspectors performed a biennial inspection of the licensees LORT test/examination  
      operating examination material consisted of 6 operating tests, each containing
program for compliance with the stations SAT program that would satisfy the  
      approximately two dynamic simulator scenarios and five job performance measures
requirements of 10 CFR 55.59(c)(4), Evaluation. The inspectors reviewed the 2006  
      (JPMs). The inspectors reviewed the annual requalification operating test and biennial
biennial written requalification examinations and 2007 annual operating test material to  
      written examination material to evaluate general quality, construction, and difficulty level.
evaluate general quality, construction, and difficulty level. The written examinations  
      The inspectors assessed the level of examination material duplication from week-to-
reviewed consisted of four written examinations, each containing 30 questions. The  
      week during the current year operating test and written examinations. The inspectors
operating examination material consisted of 6 operating tests, each containing  
      reviewed the methodology for developing the examinations, including the LORT program
approximately two dynamic simulator scenarios and five job performance measures  
      two-year sample plan, probabilistic risk assessment insights, previously identified
(JPMs). The inspectors reviewed the annual requalification operating test and biennial  
      operator performance deficiencies, and plant modifications.
written examination material to evaluate general quality, construction, and difficulty level.
  b. Findings
The inspectors assessed the level of examination material duplication from week-to-
      No findings of significance were identified.
week during the current year operating test and written examinations. The inspectors  
.4   Licensee Administration of Requalification Examinations
reviewed the methodology for developing the examinations, including the LORT program  
  a. Inspection Scope
two-year sample plan, probabilistic risk assessment insights, previously identified  
      The inspectors observed the administration of a requalification operating test to assess
operator performance deficiencies, and plant modifications.  
      the licensees effectiveness in conducting the test to ensure compliance with
b.  
      10 CFR 55.59(c)(4), Evaluation. The inspectors evaluated the performance of one
Findings  
      crew in parallel with the facility evaluators during one dynamic simulator scenario and
No findings of significance were identified.  
      evaluated various licensed crew members concurrently with facility evaluators during the
.4  
      administration of several JPMs. The inspectors assessed the facility evaluators ability
Licensee Administration of Requalification Examinations  
      to determine adequate crew and individual performance using objective, measurable
a.  
      standards. The inspectors observed the training staff personnel administer the operating
Inspection Scope  
      test, including conducting pre-examination briefings, evaluations of operator
The inspectors observed the administration of a requalification operating test to assess  
      performance, and individual and crew evaluations upon completion of the operating test.
the licensees effectiveness in conducting the test to ensure compliance with  
      The inspectors evaluated the ability of the simulator to support the examinations. A
10 CFR 55.59(c)(4), Evaluation. The inspectors evaluated the performance of one  
      specific evaluation of simulator performance was conducted and documented under
crew in parallel with the facility evaluators during one dynamic simulator scenario and  
      Section 1R11.9 of this report.
evaluated various licensed crew members concurrently with facility evaluators during the  
                                                12                                    Enclosure
administration of several JPMs. The inspectors assessed the facility evaluators ability  
to determine adequate crew and individual performance using objective, measurable  
standards. The inspectors observed the training staff personnel administer the operating  
test, including conducting pre-examination briefings, evaluations of operator  
performance, and individual and crew evaluations upon completion of the operating test.
The inspectors evaluated the ability of the simulator to support the examinations. A  
specific evaluation of simulator performance was conducted and documented under  
Section 1R11.9 of this report.


  b. Findings
    No findings of significance were identified.
13
.5   Examination Security
Enclosure
  a. Inspection Scope
b.  
    The inspectors observed and reviewed the licensees overall licensed operator
Findings  
    requalification examination security program related to examination physical security
No findings of significance were identified.  
    (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability
.5  
    and bias) to verify compliance with 10 CFR 55.49, Integrity of examinations and tests.
Examination Security  
    The inspectors also reviewed the facility licensees examination security procedure, any
a.  
    corrective actions related to past or present examination security problems at the facility,
Inspection Scope  
    and the implementation of security and integrity measures (e.g., security agreements,
The inspectors observed and reviewed the licensees overall licensed operator  
    sampling criteria, bank use, and test item repetition) throughout the examination
requalification examination security program related to examination physical security  
    process.
(e.g., access restrictions and simulator considerations) and integrity (e.g., predictability  
  b. Findings
and bias) to verify compliance with 10 CFR 55.49, Integrity of examinations and tests.
    There was one issue associated with examination security identified by the licensee
The inspectors also reviewed the facility licensees examination security procedure, any  
    during the administration of JPMs during the sixth week of administration of the 2007
corrective actions related to past or present examination security problems at the facility,  
    annual operating test. On October 31, 2007, an individual who had just completed a
and the implementation of security and integrity measures (e.g., security agreements,  
    simulator JPM was escorted back to the waiting room area and dropped off. However,
sampling criteria, bank use, and test item repetition) throughout the examination  
    there was no examination sequesterer in the waiting room area to ensure that there was
process.  
    no examination compromise with individuals in the room who had not been administered
b.  
    the JPM. Within two minutes, the licensee identified the potential for an examination
Findings  
    compromise. The licensee determined that the individual who had just been
There was one issue associated with examination security identified by the licensee  
    administered the JPM did not communicate any exam-related information to any other
during the administration of JPMs during the sixth week of administration of the 2007  
    individuals who had not been administered the JPM. As part of its corrective actions, the
annual operating test. On October 31, 2007, an individual who had just completed a  
    licensee held a training department standdown with the members of the examination
simulator JPM was escorted back to the waiting room area and dropped off. However,  
    team. The licensee replaced the JPM in question for the remaining individuals to be
there was no examination sequesterer in the waiting room area to ensure that there was  
    tested. The issue was documented in the corrective action program as CAP 01115710.
no examination compromise with individuals in the room who had not been administered  
    The NRC was appropriately notified of the issue. The issue was reviewed and assessed
the JPM. Within two minutes, the licensee identified the potential for an examination  
    for a possible violation of 10 CFR 55.49, Integrity of examinations and tests. With the
compromise. The licensee determined that the individual who had just been  
    actions taken, it was determined that no actual examination compromise had occurred.
administered the JPM did not communicate any exam-related information to any other  
    The issue was not subject to enforcement action in accordance with NRC enforcement
individuals who had not been administered the JPM. As part of its corrective actions, the  
    policy.
licensee held a training department standdown with the members of the examination  
.6   Licensee Training Feedback System
team. The licensee replaced the JPM in question for the remaining individuals to be  
  a. Inspection Scope
tested. The issue was documented in the corrective action program as CAP 01115710.
    The inspectors assessed the methods and effectiveness of the licensees processes
The NRC was appropriately notified of the issue. The issue was reviewed and assessed  
    for revising and maintaining its LORT program up-to-date, including the use of feedback
for a possible violation of 10 CFR 55.49, Integrity of examinations and tests. With the  
    from plant events and industry experience information. The inspectors reviewed the
actions taken, it was determined that no actual examination compromise had occurred.
    licensees quality assurance oversight activities, including licensee training department
The issue was not subject to enforcement action in accordance with NRC enforcement  
    self-assessment reports. The inspectors evaluated the licensees ability to assess the
policy.  
    effectiveness of its LORT program and its ability to implement appropriate corrective
.6  
                                              13                                        Enclosure
Licensee Training Feedback System  
a.  
Inspection Scope  
The inspectors assessed the methods and effectiveness of the licensees processes  
for revising and maintaining its LORT program up-to-date, including the use of feedback  
from plant events and industry experience information. The inspectors reviewed the  
licensees quality assurance oversight activities, including licensee training department  
self-assessment reports. The inspectors evaluated the licensees ability to assess the  
effectiveness of its LORT program and its ability to implement appropriate corrective  


      actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c)
      Requalification program requirements, and the licensees SAT program.
14
  b. Findings
Enclosure
      No findings of significance were identified.
actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c)  
.7   Licensee Remedial Training Program
Requalification program requirements, and the licensees SAT program.  
  a. Inspection Scope
b.  
      The inspectors assessed the adequacy and effectiveness of the remedial training
Findings  
      conducted since the previous biennial requalification examinations and the training from
No findings of significance were identified.  
      the current examination cycle to ensure that they addressed weaknesses in licensed
.7  
      operator or crew performance identified during training and plant operations. The
Licensee Remedial Training Program  
      inspectors reviewed remedial training procedures and individual remedial training plans.
a.  
      This evaluation was performed in accordance with 10 CFR 55.59(c), Requalification
Inspection Scope  
      program requirements, and with respect to the licensees SAT program.
The inspectors assessed the adequacy and effectiveness of the remedial training  
  b. Findings
conducted since the previous biennial requalification examinations and the training from  
      No findings of significance were identified.
the current examination cycle to ensure that they addressed weaknesses in licensed  
.8   Conformance with Operator License Conditions
operator or crew performance identified during training and plant operations. The  
  a. Inspection Scope
inspectors reviewed remedial training procedures and individual remedial training plans.
      The inspectors reviewed the facility and individual operator licensees' conformance
This evaluation was performed in accordance with 10 CFR 55.59(c), Requalification  
      with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's
program requirements, and with respect to the licensees SAT program.  
      program for maintaining active operator licenses and to assess compliance with
b.  
      10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the
Findings  
      process for tracking on-shift hours for licensed operators and which control room
No findings of significance were identified.  
      positions were granted watch-standing credit for maintaining active operator licenses.
.8  
      The inspectors reviewed the facility licensee's LORT program to assess compliance with
Conformance with Operator License Conditions  
      the requalification program requirements as described by 10 CFR 55.59(c). Additionally,
  a. Inspection Scope  
      medical records for seven licensed operators were reviewed for compliance with
The inspectors reviewed the facility and individual operator licensees' conformance  
      10 CFR 55.53(i).
with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's  
  b. Findings
program for maintaining active operator licenses and to assess compliance with  
      No findings of significance were identified.
10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the  
.9   Conformance with Simulator Requirements
process for tracking on-shift hours for licensed operators and which control room  
  a. Inspection Scope
positions were granted watch-standing credit for maintaining active operator licenses.
      The inspectors assessed the adequacy of the licensees simulation facility (simulator) for
The inspectors reviewed the facility licensee's LORT program to assess compliance with  
      use in operator licensing examinations and for satisfying experience requirements as
the requalification program requirements as described by 10 CFR 55.59(c). Additionally,  
      prescribed in 10 CFR 55.46, Simulation facilities. The inspectors also reviewed a
medical records for seven licensed operators were reviewed for compliance with  
      sample of simulator performance test records (i.e., transient tests, malfunction tests, and
10 CFR 55.53(i).  
      core performance tests), simulator discrepancies, and the process for ensuring
  b. Findings  
                                                14                                    Enclosure
No findings of significance were identified.  
.9  
Conformance with Simulator Requirements  
a.  
Inspection Scope  
The inspectors assessed the adequacy of the licensees simulation facility (simulator) for  
use in operator licensing examinations and for satisfying experience requirements as  
prescribed in 10 CFR 55.46, Simulation facilities. The inspectors also reviewed a  
sample of simulator performance test records (i.e., transient tests, malfunction tests, and  
core performance tests), simulator discrepancies, and the process for ensuring  


      continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The
      inspectors reviewed and evaluated the discrepancy process to ensure that simulator
15
      fidelity was maintained. Open simulator discrepancies were reviewed for importance
Enclosure
      relative to the impact on 10 CFR 55.45 and 55.59 operator actions, as well as on nuclear
continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The  
      and thermal hydraulic operating characteristics. The inspectors interviewed the
inspectors reviewed and evaluated the discrepancy process to ensure that simulator  
      licensees simulator staff about the configuration control process and completed the
fidelity was maintained. Open simulator discrepancies were reviewed for importance  
      Inspection Procedure 71111.11, Appendix C checklist, to evaluate whether the
relative to the impact on 10 CFR 55.45 and 55.59 operator actions, as well as on nuclear  
      licensees plant-referenced simulator was operating adequately as required by
and thermal hydraulic operating characteristics. The inspectors interviewed the  
      10 CFR 55.46(c) and (d).
licensees simulator staff about the configuration control process and completed the  
  b. Findings
Inspection Procedure 71111.11, Appendix C checklist, to evaluate whether the  
      No findings of significance were identified.
licensees plant-referenced simulator was operating adequately as required by  
.10 Annual Operating Test Results
10 CFR 55.46(c) and (d).  
  a. Inspection Scope
b.  
      The inspectors reviewed the overall pass/fail results of the annual JPM operating tests,
Findings  
      and the annual simulator operating tests (required to be given per 10 CFR 55.59(a)(2))
No findings of significance were identified.  
      administered by the licensee during 2007. The overall results were compared with the
.10  
      SDP in accordance with IMC 0609, Appendix I, Operator Requalification Human
Annual Operating Test Results  
      Performance Significance Determination Process (SDP), dated August 22, 2005. The
a.  
      year 2007 was the first year of the licensees 24-month training program; therefore, no
Inspection Scope  
      written examination was administered in 2007.
The inspectors reviewed the overall pass/fail results of the annual JPM operating tests,  
      This represented one sample.
and the annual simulator operating tests (required to be given per 10 CFR 55.59(a)(2))  
  b. Findings
administered by the licensee during 2007. The overall results were compared with the  
      No findings of significance were identified.
SDP in accordance with IMC 0609, Appendix I, Operator Requalification Human  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
Performance Significance Determination Process (SDP), dated August 22, 2005. The  
  a. Inspection Scope
year 2007 was the first year of the licensees 24-month training program; therefore, no  
      The inspectors reviewed risk assessments for planned and emergent maintenance
written examination was administered in 2007.  
      activities during the specified work weeks. During these reviews, the inspectors
This represented one sample.  
      compared the licensees risk management actions to those actions specified in the
b.  
      licensees procedures for the assessment and management of risk associated with
Findings  
      maintenance activities. The inspectors assessed whether evaluation, planning, control,
No findings of significance were identified.  
      and performance of the work were done in a manner to reduce the risk and minimize the
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
      duration, where practical, and whether contingency plans were in place where
a.  
      appropriate.
Inspection Scope  
      The inspectors used the licensees daily configuration risk assessment records,
The inspectors reviewed risk assessments for planned and emergent maintenance  
      observations of shift turnover meetings and observations of daily plant status meetings
activities during the specified work weeks. During these reviews, the inspectors  
      to determine whether the equipment configurations were properly listed. The inspectors
compared the licensees risk management actions to those actions specified in the  
      also verified that protected equipment was identified and controlled as appropriate and
licensees procedures for the assessment and management of risk associated with  
      that significant aspects of plant risk were communicated to the necessary personnel.
maintenance activities. The inspectors assessed whether evaluation, planning, control,  
                                                15                                    Enclosure
and performance of the work were done in a manner to reduce the risk and minimize the  
duration, where practical, and whether contingency plans were in place where  
appropriate.  
The inspectors used the licensees daily configuration risk assessment records,  
observations of shift turnover meetings and observations of daily plant status meetings  
to determine whether the equipment configurations were properly listed. The inspectors  
also verified that protected equipment was identified and controlled as appropriate and  
that significant aspects of plant risk were communicated to the necessary personnel.


      The reviews of maintenance risk assessment and emergent work evaluation constituted
      five inspection procedure samples:
16
      *       Planned and emergent maintenance during the week of October 15, 2007;
Enclosure
      *       Planned and emergent maintenance during the week of October 22;
The reviews of maintenance risk assessment and emergent work evaluation constituted  
      *       Planned and emergent maintenance during the week of October 29;
five inspection procedure samples:  
      *       Planned and emergent maintenance during the week of November 26; and
*  
      *       Planned and emergent maintenance during the week of December 10.
Planned and emergent maintenance during the week of October 15, 2007;
  b. Findings
*  
      No findings of significance were identified.
Planned and emergent maintenance during the week of October 22;
1R15 Operability Evaluations (71111.15)
*  
.1   Service Water (SW) Pump P-32C Issues
Planned and emergent maintenance during the week of October 29;
  a. Inspection Scope
*  
      The inspectors reviewed CAP 01098680, its associated operability evaluation (OPR),
Planned and emergent maintenance during the week of November 26; and  
      apparent cause evaluation (ACE), and past operability evaluation in the licensees
*  
      corrective action program. The inspectors reviewed design basis information, the FSAR,
Planned and emergent maintenance during the week of December 10.  
      TS requirements, and licensee procedures to determine the technical adequacy of the
b.  
      operability evaluations. The inspectors also reviewed the licensees implementation of
Findings  
      select sections of the American Society of Mechanical Engineers (ASME) Operational
No findings of significance were identified.  
      Maintenance (OM) Code, 1995 Addenda, to evaluate whether requirements were met
1R15 Operability Evaluations (71111.15)  
      and the appropriate actions were taken in accordance with the Code. In addition, the
.1  
      inspectors determined whether compensatory measures were implemented, as required.
Service Water (SW) Pump P-32C Issues  
      The inspectors assessed whether system operability was properly justified and that the
a.  
      system remained available, such that no unrecognized increase in risk occurred.
Inspection Scope  
      This review constituted one sample.
The inspectors reviewed CAP 01098680, its associated operability evaluation (OPR),  
  b. Findings
apparent cause evaluation (ACE), and past operability evaluation in the licensees  
      Introduction: A self-revealing finding with no associated violation of regulatory
corrective action program. The inspectors reviewed design basis information, the FSAR,  
      requirements was identified for an inadequate operability evaluation issued on
TS requirements, and licensee procedures to determine the technical adequacy of the  
      June 28, 2007, associated with safety-related SW pump P-32C. Specifically, P-32C
operability evaluations. The inspectors also reviewed the licensees implementation of  
      failed its inservice test (IST) on high vibrations after only 6.5 hours of operation, but the
select sections of the American Society of Mechanical Engineers (ASME) Operational  
      June 2007 operability evaluation had concluded that the pump would remain operable
Maintenance (OM) Code, 1995 Addenda, to evaluate whether requirements were met  
      and not reach the IST out-of-service limit until 120 hours of continuous operation. The
and the appropriate actions were taken in accordance with the Code. In addition, the  
      licensees non-conservative decision-making and use of a non-conservative prediction
inspectors determined whether compensatory measures were implemented, as required.
      model led to the incorrect conclusion of operability of the P-32C pump. Had the licensee
The inspectors assessed whether system operability was properly justified and that the  
      used an appropriate prediction model, reflective of a degraded/degrading pump, the
system remained available, such that no unrecognized increase in risk occurred.  
      OPR would have concluded the pump was inoperable.
This review constituted one sample.  
      Description: Service water pump P-32C was placed on increased IST frequency after
b.  
      trending into the IST Alert Range in May 2007. On June 24, 2007, during the next
Findings  
      performance of increased frequency testing, P-32C vibration was recorded at 0.3051
Introduction: A self-revealing finding with no associated violation of regulatory  
      inches per second (ips) compared to the Required Action limit of > 0.327 ips. Because
requirements was identified for an inadequate operability evaluation issued on  
      this vibration measurements approaching this out-of-service limit of the pump,
June 28, 2007, associated with safety-related SW pump P-32C. Specifically, P-32C  
                                                16                                      Enclosure
failed its inservice test (IST) on high vibrations after only 6.5 hours of operation, but the  
June 2007 operability evaluation had concluded that the pump would remain operable  
and not reach the IST out-of-service limit until 120 hours of continuous operation. The  
licensees non-conservative decision-making and use of a non-conservative prediction  
model led to the incorrect conclusion of operability of the P-32C pump. Had the licensee  
used an appropriate prediction model, reflective of a degraded/degrading pump, the  
OPR would have concluded the pump was inoperable.  
Description: Service water pump P-32C was placed on increased IST frequency after  
trending into the IST Alert Range in May 2007. On June 24, 2007, during the next  
performance of increased frequency testing, P-32C vibration was recorded at 0.3051  
inches per second (ips) compared to the Required Action limit of > 0.327 ips. Because  
this vibration measurements approaching this out-of-service limit of the pump,  


OPR 01098680 was performed to: review the vibration trend and determine the
additional run time until the IST out-of-service limit might be reached, compare this
17
duration to the mission time of the P-32C pump, and determine if any additional
Enclosure
compensatory measures were required to be taken.
OPR 01098680 was performed to: review the vibration trend and determine the  
Licensee engineers utilized vibration analysis software to predict the point at which
additional run time until the IST out-of-service limit might be reached, compare this  
P-32C would exceed the 0.327 ips out-of-service limit. Based on the licensees
duration to the mission time of the P-32C pump, and determine if any additional  
assumption that the degrading vibration trend was due to normal bearing wear, the trend
compensatory measures were required to be taken.  
projection grossly overestimated the pumps remaining acceptable run time.
Licensee engineers utilized vibration analysis software to predict the point at which  
Specifically, the model predicted that an additional 120 hours, or five days, of continuous
P-32C would exceed the 0.327 ips out-of-service limit. Based on the licensees  
operation could be achieved before reaching 0.327 ips. On August 8, 2007, however,
assumption that the degrading vibration trend was due to normal bearing wear, the trend  
the next increased frequency IST was performed on P-32C and a vibration level of
projection grossly overestimated the pumps remaining acceptable run time.
0.4055 ips was observed. Because this value exceeded the 0.327 ips IST out-of-service
Specifically, the model predicted that an additional 120 hours, or five days, of continuous  
limit, P-32C was declared inoperable and the appropriate TS action statement was
operation could be achieved before reaching 0.327 ips. On August 8, 2007, however,  
entered. The pump was subsequently rebuilt and returned to service on August 11 after
the next increased frequency IST was performed on P-32C and a vibration level of  
71 hours of unavailability.
0.4055 ips was observed. Because this value exceeded the 0.327 ips IST out-of-service  
The inspectors reviewed ACE 01098680-02. The purpose of this ACE was to determine
limit, P-32C was declared inoperable and the appropriate TS action statement was  
the cause of the unexpected step change in vibrations and to determine why vibrations
entered. The pump was subsequently rebuilt and returned to service on August 11 after  
exceeded the IST out-of-service limit in only 6.5 hours vice the 120 hours of predicted
71 hours of unavailability.  
run time. From the review, the inspectors concluded that the licensee applied non-
The inspectors reviewed ACE 01098680-02. The purpose of this ACE was to determine  
conservative assumptions to the vibration trend projection when it failed to factor in
the cause of the unexpected step change in vibrations and to determine why vibrations  
vibration amplifying resonance effects, or any additional conservative margin for
exceeded the IST out-of-service limit in only 6.5 hours vice the 120 hours of predicted  
uncertainty.
run time. From the review, the inspectors concluded that the licensee applied non-
The inspectors identified another example of the licensees non-conservative
conservative assumptions to the vibration trend projection when it failed to factor in  
decision-making. Specifically, the licensees OPR did not conservatively address
vibration amplifying resonance effects, or any additional conservative margin for  
the 30-day design basis mission time of the SW pumps when the IST out-of-service
uncertainty.  
limit was predicted to be reached in less than the full 30-day mission time.
The inspectors identified another example of the licensees non-conservative  
Section ISTB 6.2.2 of the Code states: If the measured test parameter values fall
decision-making. Specifically, the licensees OPR did not conservatively address  
within the required action range, the pump shall be declared inoperable until either
the 30-day design basis mission time of the SW pumps when the IST out-of-service  
the cause of the deviation has been determined and the condition is corrected, or an
limit was predicted to be reached in less than the full 30-day mission time.
analysis of the pump is performed and new reference values are established in
Section ISTB 6.2.2 of the Code states: If the measured test parameter values fall  
accordance with paragraph ISTB 4.6. of the Code. The licensee did not declare
within the required action range, the pump shall be declared inoperable until either  
P-32C inoperable when it was identified that the vibration parameters would exceed the
the cause of the deviation has been determined and the condition is corrected, or an  
required action limit within the 30-day mission time of the pump, nor were new baseline
analysis of the pump is performed and new reference values are established in  
values established in accordance with the Code.
accordance with paragraph ISTB 4.6. of the Code. The licensee did not declare  
Analysis: The inspectors determined that the failure to use appropriate, conservative,
P-32C inoperable when it was identified that the vibration parameters would exceed the  
calculation assumptions in the trend projection to justify the basis for the continued
required action limit within the 30-day mission time of the pump, nor were new baseline  
operability of a safety-related-pump, is a performance deficiency and a finding. The
values established in accordance with the Code.
finding is more than minor because it could reasonably be viewed as a precursor to a
Analysis: The inspectors determined that the failure to use appropriate, conservative,  
significant event.
calculation assumptions in the trend projection to justify the basis for the continued  
Using IMC 0609, Significance Determination Process, dated January 10, 2008, the
operability of a safety-related-pump, is a performance deficiency and a finding. The  
inspectors determined that the finding is of very low safety significance (Green) because
finding is more than minor because it could reasonably be viewed as a precursor to a  
the finding did not involve a design deficiency, there was no actual loss of safety
significant event.  
function, no single train loss of safety function for greater than the TS-allowed outage
Using IMC 0609, Significance Determination Process, dated January 10, 2008, the  
time, and no risk due to external events.
inspectors determined that the finding is of very low safety significance (Green) because  
                                          17                                      Enclosure
the finding did not involve a design deficiency, there was no actual loss of safety  
function, no single train loss of safety function for greater than the TS-allowed outage  
time, and no risk due to external events.  


    Additionally, the inspectors determined that the finding had a cross-cutting aspect in the
    area of human performance. Specifically, the licensee failed to use conservative
18
    assumptions in making decisions affecting the operability of safety-related components
Enclosure
    (H.1(b)).
Additionally, the inspectors determined that the finding had a cross-cutting aspect in the  
    Enforcement: The failure to perform an adequate operability evaluation, which was
area of human performance. Specifically, the licensee failed to use conservative  
    based upon non-conservative decision-making and a non-conservative trend projection,
assumptions in making decisions affecting the operability of safety-related components  
    was not a violation of regulatory requirements although a performance deficiency
(H.1(b)).  
    existed. Therefore, this issue is considered a finding of very low safety significance
Enforcement: The failure to perform an adequate operability evaluation, which was  
    (FIN 05000266/2007005-02; 05000301/2007005-02).
based upon non-conservative decision-making and a non-conservative trend projection,  
    The licensee included this finding in its corrective action program as CAP 01119241 and
was not a violation of regulatory requirements although a performance deficiency  
    has actions planned to perform an ACE to address the use of IST trend data in OPRs.
existed. Therefore, this issue is considered a finding of very low safety significance  
.2   Operability Evaluations for the Unit 2 TDAFW Pump 2P-29 Following Overhaul
(FIN 05000266/2007005-02; 05000301/2007005-02).  
  a. Inspection Scope
The licensee included this finding in its corrective action program as CAP 01119241 and  
    The inspectors reviewed selected immediate operability evaluations and operability
has actions planned to perform an ACE to address the use of IST trend data in OPRs.  
    evaluations associated with issues entered into the licensees corrective action program.
.2  
    The inspectors reviewed design basis information, the FSAR, TS requirements, and
Operability Evaluations for the Unit 2 TDAFW Pump 2P-29 Following Overhaul
    licensee procedures to determine the technical adequacy of the operability evaluations.
a.  
    In addition, the inspectors determined whether compensatory measures were
Inspection Scope  
    implemented, as required. The inspectors assessed whether system operability was
The inspectors reviewed selected immediate operability evaluations and operability  
    properly justified and that the system remained available, such that no unrecognized
evaluations associated with issues entered into the licensees corrective action program.
    increase in risk occurred.
The inspectors reviewed design basis information, the FSAR, TS requirements, and  
    The reviews of the following OPRs constituted six samples:
licensee procedures to determine the technical adequacy of the operability evaluations.
    *       CAP 01112660, 2P-29 Outboard Bearing Water Following IT-09A, dated
In addition, the inspectors determined whether compensatory measures were  
              September 24, 2007;
implemented, as required. The inspectors assessed whether system operability was  
    *       CAP 01113318, IT-09A Oil Analysis Results Not as Expected for 2P-29, dated
properly justified and that the system remained available, such that no unrecognized  
              September 27, 2007;
increase in risk occurred.  
    *       OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,
The reviews of the following OPRs constituted six samples:
              Revision 2, dated November 3, 2007;
*  
    *       OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,
CAP 01112660, 2P-29 Outboard Bearing Water Following IT-09A, dated  
              Revision 3, dated November 4, 2007;
September 24, 2007;  
    *       OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,
*  
              Revision 4, dated November 7, 2007; and
CAP 01113318, IT-09A Oil Analysis Results Not as Expected for 2P-29, dated  
    *       OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,
September 27, 2007;  
              Revision 5, dated November 10, 2007.
*  
  b. Findings
OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,  
    Introduction: The inspectors identified a finding of very low safety significance (Green)
Revision 2, dated November 3, 2007;  
    and an associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion V,
*  
    Instructions, Procedures, and Drawings, for the failure to adequately assess operability
OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,  
    of the Unit 2 TDAFW pump in accordance with plant procedures. The inspectors
Revision 3, dated November 4, 2007;  
    identified that the licensee failed to implement procedural requirements regarding the
*  
    immediate assessment of operability on September 24 and September 27, 2007, for the
OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,  
                                                18                                    Enclosure
Revision 4, dated November 7, 2007; and  
*  
OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,  
Revision 5, dated November 10, 2007.  
b.  
Findings  
Introduction: The inspectors identified a finding of very low safety significance (Green)  
and an associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion V,  
Instructions, Procedures, and Drawings, for the failure to adequately assess operability  
of the Unit 2 TDAFW pump in accordance with plant procedures. The inspectors  
identified that the licensee failed to implement procedural requirements regarding the  
immediate assessment of operability on September 24 and September 27, 2007, for the  


increased water ingress into the turbine outboard bearing housing for the pump following
maintenance.
19
Description: On September 24, 2007, following the overhaul of the 2P-29 TDAFW
Enclosure
pump, an oil sample was taken from the outboard bearing housing, after a four-hour
increased water ingress into the turbine outboard bearing housing for the pump following  
run. CAP 01112660 was written, which documented that an estimated water volume in
maintenance.  
the oil sample based on visual indication was approximately 1,000 to 1,500 parts per
Description: On September 24, 2007, following the overhaul of the 2P-29 TDAFW  
million (ppm) for the four-hour run. The CAP description concluded that this was an
pump, an oil sample was taken from the outboard bearing housing, after a four-hour  
expected condition. A second shorter pump run was performed and the water content in
run. CAP 01112660 was written, which documented that an estimated water volume in  
the oil was visually estimated to be approximately 100 ppm of water. The licensee
the oil sample based on visual indication was approximately 1,000 to 1,500 parts per  
rationalized that the initial water content was expected and the condition report was
million (ppm) for the four-hour run. The CAP description concluded that this was an  
closed with no further actions taken. However, the inspectors identified that neither the
expected condition. A second shorter pump run was performed and the water content in  
operations nor engineering staff questioned why a visual estimate for indication of water
the oil was visually estimated to be approximately 100 ppm of water. The licensee  
in the oil would have produced five times the amount of water in the oil immediately
rationalized that the initial water content was expected and the condition report was  
following the overhaul, as compared to the first oil sample taken in June 2007 following a
closed with no further actions taken. However, the inspectors identified that neither the  
November 2006 overhaul, which showed 300 ppm water in the oil. The June 2007
operations nor engineering staff questioned why a visual estimate for indication of water  
outboard oil sample for the 2P-29 turbine was the first time the oil was sampled since the
in the oil would have produced five times the amount of water in the oil immediately  
November 2006 overhaul and the first time water ingress was noted in the turbine
following the overhaul, as compared to the first oil sample taken in June 2007 following a  
outboard bearing.
November 2006 overhaul, which showed 300 ppm water in the oil. The June 2007  
On September 27, CAP 01113318 was written and documented that the outboard oil
outboard oil sample for the 2P-29 turbine was the first time the oil was sampled since the  
sample from the first four-hour run, analyzed by a laboratory, contained 20,040 ppm of
November 2006 overhaul and the first time water ingress was noted in the turbine  
water (approximately two percent by volume). The CAP description also noted that the
outboard bearing.  
number was not consistent with the visual estimate from September 24 of 1,000 to
On September 27, CAP 01113318 was written and documented that the outboard oil  
1,500 ppm. However, the CAP dismissed the results, based on conjecture, concluding
sample from the first four-hour run, analyzed by a laboratory, contained 20,040 ppm of  
that the 20,040 ppm results were false readings due to a laboratory error or an
water (approximately two percent by volume). The CAP description also noted that the  
accidental capture of water droplets during the sampling process. The CAP concluded
number was not consistent with the visual estimate from September 24 of 1,000 to  
that the indicated levels of water in the IT-09A sample are errant. The immediate
1,500 ppm. However, the CAP dismissed the results, based on conjecture, concluding  
operability assessment concluded that based on the information provided in the
that the 20,040 ppm results were false readings due to a laboratory error or an  
description section there were no operability concerns. In addition, the assessment
accidental capture of water droplets during the sampling process. The CAP concluded  
discussed that the pump was tested satisfactorily, with no abnormal indications observed
that the indicated levels of water in the IT-09A sample are errant. The immediate  
during the run. The inspectors, as well as the licensee personnel performing the causal
operability assessment concluded that based on the information provided in the  
evaluation for this issue, concluded that the increased water first observed on
description section there were no operability concerns. In addition, the assessment  
September 24 should not have been discounted and was discounted due to
discussed that the pump was tested satisfactorily, with no abnormal indications observed  
confirmational biases, resulting in nonconservative assumptions in the evaluation of this
during the run. The inspectors, as well as the licensee personnel performing the causal  
condition.
evaluation for this issue, concluded that the increased water first observed on  
The inspectors reviewed the licensees procedure for operability, Fleet Procedure
September 24 should not have been discounted and was discounted due to  
FP OP-OL-01, Operability Determination. The procedure required a determination if
confirmational biases, resulting in nonconservative assumptions in the evaluation of this  
a condition existed that could call into question the ability of a structure, system, or
condition.  
component (SSC) to perform its specified safety function. An example of such a
The inspectors reviewed the licensees procedure for operability, Fleet Procedure  
condition was an item which met the definition of a degraded condition. A degraded
FP OP-OL-01, Operability Determination. The procedure required a determination if  
condition, as defined in the fleet procedure, was a condition where there had been a
a condition existed that could call into question the ability of a structure, system, or  
noticeable change in parameters that were precursors to failure. The attachment
component (SSC) to perform its specified safety function. An example of such a  
guidance for immediate operability review also highlighted questions for performing
condition was an item which met the definition of a degraded condition. A degraded  
operability determinations, which included the following: Could the capability of a SSC
condition, as defined in the fleet procedure, was a condition where there had been a  
to prevent or mitigate consequences of an accident as postulated in the Final Safety
noticeable change in parameters that were precursors to failure. The attachment  
Analysis Report be reduced? The guidance suggested that an OPR should be
guidance for immediate operability review also highlighted questions for performing  
requested if additional engineering evaluation and justification was needed to answer
operability determinations, which included the following: Could the capability of a SSC  
those questions. Finally, the inspectors noted that the guidelines for operability
to prevent or mitigate consequences of an accident as postulated in the Final Safety  
recommendations included guidance to evaluate trend data to identify a deteriorating
Analysis Report be reduced? The guidance suggested that an OPR should be  
                                          19                                      Enclosure
requested if additional engineering evaluation and justification was needed to answer  
those questions. Finally, the inspectors noted that the guidelines for operability  
recommendations included guidance to evaluate trend data to identify a deteriorating  


condition and to utilize an OPR to predict the point when a SSC may become
inoperable. The inspectors concluded the licensee had not adequately implemented the
20
procedures for operability determinations for the September 24 and 27 CAPs. The
Enclosure
licensee had not assessed the parameter of a significant increase in the ingress of water
condition and to utilize an OPR to predict the point when a SSC may become  
following a maintenance overhaul, as compared to the last maintenance overhaul.
inoperable. The inspectors concluded the licensee had not adequately implemented the  
On November 1, 2007, approximately 5 weeks after the maintenance overhaul, the
procedures for operability determinations for the September 24 and 27 CAPs. The  
licensee ran 2P-29 for about two hours and then sampled the oil. The outboard oil
licensee had not assessed the parameter of a significant increase in the ingress of water  
sample had 29,515 ppm of water in the oil. The licensee declared the pump inoperable
following a maintenance overhaul, as compared to the last maintenance overhaul.  
and revised the July 2007 operability evaluation for the original water ingress issue in
On November 1, 2007, approximately 5 weeks after the maintenance overhaul, the  
June.
licensee ran 2P-29 for about two hours and then sampled the oil. The outboard oil  
On November 3, the licensee issued Revision 2 to OPR1098358 and the pump was
sample had 29,515 ppm of water in the oil. The licensee declared the pump inoperable  
determined to be capable of performing the design functions for the design basis mission
and revised the July 2007 operability evaluation for the original water ingress issue in  
time of eight hours. On November 4, Revision 3 to OPR1098358 was issued to specify
June.  
a compensatory measure of testing the pump every 72 hours for an eight-hour duration.
On November 3, the licensee issued Revision 2 to OPR1098358 and the pump was  
The subsequent pump runs continued to show high levels of water in the outboard
determined to be capable of performing the design functions for the design basis mission  
bearing oil. The inspectors identified that Revisions 2 and 3 utilized data from 2P-29 on
time of eight hours. On November 4, Revision 3 to OPR1098358 was issued to specify  
water ingress rates prior to the September 2007 turbine overhaul. These values were
a compensatory measure of testing the pump every 72 hours for an eight-hour duration.
not applicable to the current condition, because the September maintenance had
The subsequent pump runs continued to show high levels of water in the outboard  
created a new and greater water ingress problem. Revision 4 to OPR1098358, issued
bearing oil. The inspectors identified that Revisions 2 and 3 utilized data from 2P-29 on  
on November 7, was a rewrite of the OPR utilizing current oil analysis data from after the
water ingress rates prior to the September 2007 turbine overhaul. These values were  
overhaul. In addition, the licensee hypothesized, as part of the operability discussion,
not applicable to the current condition, because the September maintenance had  
that differences in water concentrations in the oil seen since November 1 were likely the
created a new and greater water ingress problem. Revision 4 to OPR1098358, issued  
result of a change in sampling techniques. However, the inspectors noted that these
on November 7, was a rewrite of the OPR utilizing current oil analysis data from after the  
theories were refuted by visual observation and comparison of the quarantined oil
overhaul. In addition, the licensee hypothesized, as part of the operability discussion,  
samples taken since November 1. Further testing of the previous oil samples also
that differences in water concentrations in the oil seen since November 1 were likely the  
refuted the sampling technique theories. In addition, the inspectors noted that the
result of a change in sampling techniques. However, the inspectors noted that these  
licensee did not have any established procedural controls or work instructions for mixing
theories were refuted by visual observation and comparison of the quarantined oil  
of the samples and splitting of the samples to ensure quality control. The licensee
samples taken since November 1. Further testing of the previous oil samples also  
initiated a condition report and took immediate corrective actions to address this latter
refuted the sampling technique theories. In addition, the inspectors noted that the  
issue. Revision 5 to the OPR was issued on November 10 and contained additional
licensee did not have any established procedural controls or work instructions for mixing  
discussion on the potential for an unexpected increase in steam leakage, and additional
of the samples and splitting of the samples to ensure quality control. The licensee  
information related to the sampling technique and testing duration.
initiated a condition report and took immediate corrective actions to address this latter  
The inspectors noted that for all the revisions, the OPR demonstrated that the TDAFW
issue. Revision 5 to the OPR was issued on November 10 and contained additional  
pump would have performed the required safety functions for the eight-hour mission time
discussion on the potential for an unexpected increase in steam leakage, and additional  
of the FSAR Chapter 14 design basis accidents. However, the inspectors pointed out to
information related to the sampling technique and testing duration.  
the licensee that the OPR did not address all the safety functions required to be
The inspectors noted that for all the revisions, the OPR demonstrated that the TDAFW  
performed by the TDAFW pump, which at Point Beach included several fire-related
pump would have performed the required safety functions for the eight-hour mission time  
scenarios. The licensee subsequently initiated a CAP for this issue.
of the FSAR Chapter 14 design basis accidents. However, the inspectors pointed out to  
Additional information regarding the issues associated with the 2P-29 TDAFW pump is
the licensee that the OPR did not address all the safety functions required to be  
documented in Section 4OA5.2 of this report.
performed by the TDAFW pump, which at Point Beach included several fire-related  
Analysis: The inspectors determined that the failure to adequately perform an operability
scenarios. The licensee subsequently initiated a CAP for this issue.  
determination was a performance deficiency and a finding that warranted a significance
Additional information regarding the issues associated with the 2P-29 TDAFW pump is  
evaluation. Using IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue
documented in Section 4OA5.2 of this report.  
Screening, dated September 20, 2007, the inspectors determined that the finding is
Analysis: The inspectors determined that the failure to adequately perform an operability  
more than minor because, if left uncorrected, the failure to properly assess operability
determination was a performance deficiency and a finding that warranted a significance  
                                        20                                      Enclosure
evaluation. Using IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue  
Screening, dated September 20, 2007, the inspectors determined that the finding is  
more than minor because, if left uncorrected, the failure to properly assess operability  


    would result in the TDAFW pump being degraded and potentially inoperable, exceeding
    the allowed outage time in accordance with TSs.
21
    Using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection
Enclosure
    Findings for At-Power Situations, dated January 10, 2008, the inspectors determined
would result in the TDAFW pump being degraded and potentially inoperable, exceeding  
    the finding may have resulted in a late determination of an actual loss of safety function
the allowed outage time in accordance with TSs.  
    of a system or train of equipment. The risk assessment for the potential loss of safety
Using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection  
    function is attributed to the performance deficiencies associated with inadequate
Findings for At-Power Situations, dated January 10, 2008, the inspectors determined  
    maintenance discussed in Section 4OA5.2.b.2 as URI 5000266/2007005-07. This did
the finding may have resulted in a late determination of an actual loss of safety function  
    not cause the loss of safety function for greater than the allowed outage time.
of a system or train of equipment. The risk assessment for the potential loss of safety  
    Therefore, the finding is considered to be of very low safety significance (Green).
function is attributed to the performance deficiencies associated with inadequate  
    Additionally, the inspectors determined that the finding has a cross-cutting aspect in the
maintenance discussed in Section 4OA5.2.b.2 as URI 5000266/2007005-07. This did  
    area of human performance. Specifically, the licensee failed to use conservative
not cause the loss of safety function for greater than the allowed outage time.
    assumptions in decision-making affecting operability of safety-related equipment
Therefore, the finding is considered to be of very low safety significance (Green).
    (H.1(b)).
Additionally, the inspectors determined that the finding has a cross-cutting aspect in the  
    Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures,
area of human performance. Specifically, the licensee failed to use conservative  
    and Drawings, requires, in part, that activities affecting quality be prescribed and
assumptions in decision-making affecting operability of safety-related equipment  
    accomplished by procedures appropriate to the circumstances. The licensee failed
(H.1(b)).  
    to implement the operability determination procedure FP-OP-OL-01, Operability
Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures,  
    Determination. The procedure required, in part, that the licensee assess the
and Drawings, requires, in part, that activities affecting quality be prescribed and  
    capability of a SSC to prevent or mitigate consequences of an accident as
accomplished by procedures appropriate to the circumstances. The licensee failed  
    postulated in the FSAR. Contrary to this, the licensee failed to adequately assess
to implement the operability determination procedure FP-OP-OL-01, Operability  
    the operability of the turbine outboard bearing for the Unit 2 TDAFW pump following
Determination. The procedure required, in part, that the licensee assess the  
    increased water intrusion during post-maintenance testing on September 24, 2007,
capability of a SSC to prevent or mitigate consequences of an accident as  
    and later corroborated by oil analyses on September 27. Because this finding was of
postulated in the FSAR. Contrary to this, the licensee failed to adequately assess  
    very low safety significance (Green) and because it was entered into the licensees
the operability of the turbine outboard bearing for the Unit 2 TDAFW pump following  
    corrective action program (as CAP 01115748), this violation is being treated as a
increased water intrusion during post-maintenance testing on September 24, 2007,  
    Non-Cited Violation, consistent with Section VI.A of the NRC Enforcement Policy
and later corroborated by oil analyses on September 27. Because this finding was of  
    (NCV 05000301/2007005-03).
very low safety significance (Green) and because it was entered into the licensees  
    The licensee took immediate corrective actions to address the issue, and at the end of
corrective action program (as CAP 01115748), this violation is being treated as a  
    the inspection period the licensee continued to evaluate the causes associated with this
Non-Cited Violation, consistent with Section VI.A of the NRC Enforcement Policy  
    finding.
(NCV 05000301/2007005-03).  
.3   Operability Evaluations
The licensee took immediate corrective actions to address the issue, and at the end of  
  a. Inspection Scope
the inspection period the licensee continued to evaluate the causes associated with this  
    The inspectors reviewed selected operability evaluations associated with issues entered
finding.  
    into the licensees corrective action program. The inspectors reviewed design basis
.3  
    information, the FSAR, TS requirements, and licensee procedures to determine the
Operability Evaluations  
    technical adequacy of the operability evaluations. In addition, the inspectors determined
a.  
    whether compensatory measures were implemented, as required. The inspectors
Inspection Scope  
    assessed whether system operability was properly justified and that the system
The inspectors reviewed selected operability evaluations associated with issues entered  
    remained available, such that no unrecognized increase in risk occurred.
into the licensees corrective action program. The inspectors reviewed design basis  
                                              21                                        Enclosure
information, the FSAR, TS requirements, and licensee procedures to determine the  
technical adequacy of the operability evaluations. In addition, the inspectors determined  
whether compensatory measures were implemented, as required. The inspectors  
assessed whether system operability was properly justified and that the system  
remained available, such that no unrecognized increase in risk occurred.  


      The reviews of the following operability evaluations constituted four samples:
      *       CAP 00889745, Degraded Grid Voltage Concerns;
22
      *       CAP 01111251, Discrepancy in Control Room Accident Fan Brake Horsepower
Enclosure
              Versus Vendor Data Used in Calculation 2004-0002, Revision 6;
The reviews of the following operability evaluations constituted four samples:  
      *       CAP 01114308, Unit 1 and 2 Safety Injection Valves 850A/B, Sump B Suction
*  
              Valve Limit Switches; and
CAP 00889745, Degraded Grid Voltage Concerns;  
      *       CAP 01116453, Unit 2 W-3B Control Rod Drive Shroud Fan Tripped on
*  
              Overcurrent.
CAP 01111251, Discrepancy in Control Room Accident Fan Brake Horsepower  
  b. Findings
Versus Vendor Data Used in Calculation 2004-0002, Revision 6;  
      No findings of significance were identified.
*  
1R17 Permanent Plant Modifications (71111.17)
CAP 01114308, Unit 1 and 2 Safety Injection Valves 850A/B, Sump B Suction  
.1   Annual Resident Review
Valve Limit Switches; and  
  a. Inspection Scope
*  
      The following engineering design package was reviewed and selected aspects were
CAP 01116453, Unit 2 W-3B Control Rod Drive Shroud Fan Tripped on  
      discussed with engineering personnel:
Overcurrent.  
      *       EDG G-01 and G-02 heat exchanger modification
b.  
      This document and related documentation were reviewed to assess adequacy of the
Findings  
      associated 10 CFR 50.59 safety evaluation screening; consideration of design
No findings of significance were identified.  
      parameters; implementation of the modification; post-modification testing, and proper
1R17 Permanent Plant Modifications (71111.17)  
      updating of procedures, design, and licensing documents. The inspectors observed
.1  
      ongoing and completed work activities to verify that installation was consistent with the
Annual Resident Review  
      design control documents. The modifications were installed to address a longstanding
a.  
      operator workaround for lake grass fouling of the heat exchangers.
Inspection Scope  
      This inspection constituted one sample.
The following engineering design package was reviewed and selected aspects were  
  b. Findings
discussed with engineering personnel:  
      No findings of significance were identified.
*  
1R19 Post-Maintenance Testing (71111.19)
EDG G-01 and G-02 heat exchanger modification
  a. Inspection Scope
This document and related documentation were reviewed to assess adequacy of the  
      During completion of the post-maintenance test inspection procedure samples, the
associated 10 CFR 50.59 safety evaluation screening; consideration of design  
      inspectors observed in-plant activities and reviewed procedures and associated records
parameters; implementation of the modification; post-modification testing, and proper  
      to determine whether:
updating of procedures, design, and licensing documents. The inspectors observed  
      *       Testing activities satisfied the test procedure acceptance criteria;
ongoing and completed work activities to verify that installation was consistent with the  
      *       Effects of the testing were adequately addressed prior to the testing;
design control documents. The modifications were installed to address a longstanding  
      *       Measuring and test equipment calibration was current;
operator workaround for lake grass fouling of the heat exchangers.  
      *       Test equipment was within the required range and accuracy;
This inspection constituted one sample.  
                                                22                                    Enclosure
b.  
Findings  
No findings of significance were identified.  
1R19 Post-Maintenance Testing (71111.19)  
a.  
Inspection Scope  
During completion of the post-maintenance test inspection procedure samples, the  
inspectors observed in-plant activities and reviewed procedures and associated records  
to determine whether:  
*  
Testing activities satisfied the test procedure acceptance criteria;
*  
Effects of the testing were adequately addressed prior to the testing;
*  
Measuring and test equipment calibration was current;
*  
Test equipment was within the required range and accuracy;  


    *       Applicable prerequisites described in the test procedures were satisfied;
    *       Affected systems or components were removed from service in accordance with
23
              approved procedures;
Enclosure
    *       Testing activities were performed in accordance with the test procedures and
*  
              other applicable procedures;
Applicable prerequisites described in the test procedures were satisfied;  
    *       Jumpers and lifted leads were controlled and restored where used;
*  
    *       Test data and results were accurate, complete, and valid;
Affected systems or components were removed from service in accordance with  
    *       Test equipment was removed after testing;
approved procedures;  
    *       Equipment was returned to a position or status required to support the operability
*  
              of the system in accordance with approved procedures; and
Testing activities were performed in accordance with the test procedures and  
    *       All problems identified during the testing were appropriately entered into the
other applicable procedures;  
              corrective action program.
*  
    The activities listed below were reviewed by the inspectors and constituted three
Jumpers and lifted leads were controlled and restored where used;  
    quarterly inspection procedure samples:
*  
    *       Unit 1 Charging Pump P-2A;
Test data and results were accurate, complete, and valid;
    *       Unit 1 Charging Pump P-2B Variable Frequency Drive; and
*  
    *       Service Water Pump P-32E.
Test equipment was removed after testing;
  b. Findings
*  
    No findings of significance were identified.
Equipment was returned to a position or status required to support the operability  
1R22 Surveillance Testing (71111.22)
of the system in accordance with approved procedures; and
  a. Inspection Scope
*  
    During completion of the inspection procedure samples, the inspectors observed in-plant
All problems identified during the testing were appropriately entered into the  
    activities and reviewed procedures and associated records to determine whether:
corrective action program.  
    *       Preconditioning occurred;
    *       Effects of the testing were adequately addressed by control room personnel or
The activities listed below were reviewed by the inspectors and constituted three  
              engineers prior to the commencement of the testing;
quarterly inspection procedure samples:  
    *       Acceptance criteria were clearly stated, demonstrated operational readiness, and
              were consistent with the system design basis;
*  
    *       Plant equipment calibration was correct, accurate, and properly documented; as-
Unit 1 Charging Pump P-2A;  
              left setpoints were within required ranges; and the calibration frequency were in
*  
              accordance with TSs, the FSAR, procedures, and applicable commitments;
Unit 1 Charging Pump P-2B Variable Frequency Drive; and  
    *       Measuring and test equipment calibration was current;
*  
    *       Test equipment was used within the required range and accuracy;
Service Water Pump P-32E.  
    *       Applicable prerequisites described in the test procedures were satisfied;
b.  
    *       Test frequencies met TS requirements to demonstrate operability and reliability;
Findings  
    *       Tests were performed in accordance with the test procedures and other
No findings of significance were identified.  
              applicable procedures;
1R22 Surveillance Testing (71111.22)  
    *       Jumpers and lifted leads were controlled and restored where used;
a.  
    *       Test data and results were accurate, complete, within limits, and valid;
Inspection Scope  
    *       Test equipment was removed after testing;
During completion of the inspection procedure samples, the inspectors observed in-plant  
                                                23                                      Enclosure
activities and reviewed procedures and associated records to determine whether:  
*  
Preconditioning occurred;  
*  
Effects of the testing were adequately addressed by control room personnel or  
engineers prior to the commencement of the testing;  
*  
Acceptance criteria were clearly stated, demonstrated operational readiness, and  
were consistent with the system design basis;  
*  
Plant equipment calibration was correct, accurate, and properly documented; as-
left setpoints were within required ranges; and the calibration frequency were in  
accordance with TSs, the FSAR, procedures, and applicable commitments;  
*  
Measuring and test equipment calibration was current;  
*  
Test equipment was used within the required range and accuracy;  
*  
Applicable prerequisites described in the test procedures were satisfied;  
*  
Test frequencies met TS requirements to demonstrate operability and reliability;  
*  
Tests were performed in accordance with the test procedures and other  
applicable procedures;  
*  
Jumpers and lifted leads were controlled and restored where used;  
*  
Test data and results were accurate, complete, within limits, and valid;  
*  
Test equipment was removed after testing;  


    *       Where applicable for IST activities, testing was performed in accordance with the
            applicable version of Section XI, American Society of Mechanical Engineers
24
            Code, and reference values were consistent with the system design basis;
Enclosure
    *       Where applicable, test results not meeting acceptance criteria were addressed
*  
            with an adequate operability evaluation or the system or component was
Where applicable for IST activities, testing was performed in accordance with the  
            declared inoperable;
applicable version of Section XI, American Society of Mechanical Engineers  
    *       Where applicable for safety-related instrument control surveillance tests,
Code, and reference values were consistent with the system design basis;  
            reference setting data were accurately incorporated in the test procedure;
*  
    *       Where applicable, actual conditions encountering high resistance electrical
Where applicable, test results not meeting acceptance criteria were addressed  
            contacts were such that the intended safety function could still be accomplished;
with an adequate operability evaluation or the system or component was  
    *       Prior procedure changes had not provided an opportunity to identify problems
declared inoperable;  
            encountered during the performance of the surveillance or calibration test;
*  
    *       Equipment was returned to a position or status required to support the
Where applicable for safety-related instrument control surveillance tests,  
            performance of its safety functions; and
reference setting data were accurately incorporated in the test procedure;  
    *       All problems identified during the testing were appropriately documented and
*  
            dispositioned in the corrective action program.
Where applicable, actual conditions encountering high resistance electrical  
    During this inspection period, the inspectors completed the following inspection
contacts were such that the intended safety function could still be accomplished;  
    procedure samples, which included two routine surveillances, two inservice tests, and
*  
    one containment isolation valve test, for a total of five quarterly inspection procedure
Prior procedure changes had not provided an opportunity to identify problems  
    samples:
encountered during the performance of the surveillance or calibration test;  
    *       EDG G01 surveillance testing during the week of October 22, 2007;
*  
    *       Unit 2 TDAFW pump 2P-29 ISTs on November 1 and 2;
Equipment was returned to a position or status required to support the  
    *       Unit 2 TDAFW pump 2P-29 ISTs on November 7;
performance of its safety functions; and  
    *       EDG G02 surveillance testing during the week of November 11; and
*  
    *       Testing of Unit 2 containment isolation valve SC-966.
All problems identified during the testing were appropriately documented and  
  b. Findings
dispositioned in the corrective action program.  
    No findings of significance were identified.
During this inspection period, the inspectors completed the following inspection  
1R23 Temporary Plant Modifications (71111.23)
procedure samples, which included two routine surveillances, two inservice tests, and  
  a. Inspection Scope
one containment isolation valve test, for a total of five quarterly inspection procedure  
    The inspectors reviewed the following temporary modification:
samples:  
    *       Furmanite injection of Unit 2 Moisture Separator Reheater Purge
*  
            Valve 2MS-32A.
EDG G01 surveillance testing during the week of October 22, 2007;  
    The inspectors compared the temporary configuration changes and associated
*  
    10 CFR 50.59 screening and evaluation information against the design basis, the FSAR,
Unit 2 TDAFW pump 2P-29 ISTs on November 1 and 2;  
    and the TS, as applicable, to verify that the modification did not affect the operability or
*  
    availability of the affected system. The inspectors also compared the licensees
Unit 2 TDAFW pump 2P-29 ISTs on November 7;  
    information to operating experience information to ensure that lessons learned from
*  
    other utilities had been incorporated into the licensees decision to implement the
EDG G02 surveillance testing during the week of November 11; and  
    temporary modification. The inspectors, as applicable, performed field verifications to
*  
    ensure that the modifications were installed as directed; the modifications operated as
Testing of Unit 2 containment isolation valve SC-966.  
    expected; modification testing adequately demonstrated continued system operability,
b.  
                                              24                                      Enclosure
Findings  
No findings of significance were identified.  
1R23 Temporary Plant Modifications (71111.23)  
a.  
Inspection Scope  
The inspectors reviewed the following temporary modification:  
*  
Furmanite injection of Unit 2 Moisture Separator Reheater Purge  
Valve 2MS-32A.  
The inspectors compared the temporary configuration changes and associated  
10 CFR 50.59 screening and evaluation information against the design basis, the FSAR,  
and the TS, as applicable, to verify that the modification did not affect the operability or  
availability of the affected system. The inspectors also compared the licensees  
information to operating experience information to ensure that lessons learned from  
other utilities had been incorporated into the licensees decision to implement the  
temporary modification. The inspectors, as applicable, performed field verifications to  
ensure that the modifications were installed as directed; the modifications operated as  
expected; modification testing adequately demonstrated continued system operability,  


      availability, and reliability; and that operation of the modifications did not impact the
      operability of any interfacing systems. Lastly, the inspectors discussed the temporary
25
      modification with operations, engineering, and training personnel to ensure that the
Enclosure
      individuals were aware of how extended operation with the temporary modification in
availability, and reliability; and that operation of the modifications did not impact the  
      place could impact overall plant performance.
operability of any interfacing systems. Lastly, the inspectors discussed the temporary  
      This inspection constituted one sample.
modification with operations, engineering, and training personnel to ensure that the  
  b. Findings
individuals were aware of how extended operation with the temporary modification in  
      No findings of significance were identified.
place could impact overall plant performance.  
      Cornerstone: Emergency Preparedness
This inspection constituted one sample.  
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
b.  
  a. Inspection Scope
Findings  
      The inspectors performed a screening review of the 2006 and 2007 revisions to the
No findings of significance were identified.  
      Point Beach Emergency Plan Manual to determine whether the changes decreased the
Cornerstone: Emergency Preparedness  
      plans effectiveness. This review did not constitute an approval of the changes, and as
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)  
      such, the changes are subject to future NRC inspection to ensure that the emergency
a.  
      plan continues to meet NRC regulations.
Inspection Scope  
      These activities completed one inspection sample.
The inspectors performed a screening review of the 2006 and 2007 revisions to the  
  b. Findings
Point Beach Emergency Plan Manual to determine whether the changes decreased the  
      No findings of significance were identified
plans effectiveness. This review did not constitute an approval of the changes, and as  
2.   RADIATION SAFETY
such, the changes are subject to future NRC inspection to ensure that the emergency  
      Cornerstone: Occupational Radiation Safety
plan continues to meet NRC regulations.  
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03)
These activities completed one inspection sample.  
.1   Inspection Planning
b.  
  a. Inspection Scope
Findings  
      The inspectors reviewed the FSAR to identify applicable radiation monitors associated
No findings of significance were identified  
      with measuring transient high and very high radiation areas, including those intended for
2.  
      remote emergency assessment. The inspectors identified the types of portable radiation
RADIATION SAFETY  
      detection instrumentation used for job coverage of high radiation area work, including
Cornerstone: Occupational Radiation Safety
      instruments used for underwater surveys, portable and fixed area radiation monitors
2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03)  
      used to provide radiological information in various plant areas, and continuous air
.1  
      monitors used to assess airborne radiological conditions and, consequently, work areas
Inspection Planning  
      with the potential for workers to receive a 50 millirem or greater committed effective dose
a.  
      equivalent (CEDE). Whole body counters used to monitor for internal exposure and
Inspection Scope  
      those radiation detection instruments utilized to conduct surveys for the release of
The inspectors reviewed the FSAR to identify applicable radiation monitors associated  
      personnel and equipment from the radiologically controlled area (RCA), including
with measuring transient high and very high radiation areas, including those intended for  
      contamination monitors and portal monitors, were also identified.
remote emergency assessment. The inspectors identified the types of portable radiation  
                                                  25                                      Enclosure
detection instrumentation used for job coverage of high radiation area work, including  
instruments used for underwater surveys, portable and fixed area radiation monitors  
used to provide radiological information in various plant areas, and continuous air  
monitors used to assess airborne radiological conditions and, consequently, work areas  
with the potential for workers to receive a 50 millirem or greater committed effective dose  
equivalent (CEDE). Whole body counters used to monitor for internal exposure and  
those radiation detection instruments utilized to conduct surveys for the release of  
personnel and equipment from the radiologically controlled area (RCA), including  
contamination monitors and portal monitors, were also identified.  


    These reviews represented two inspection samples.
  b. Findings
26
    No findings of significance were identified.
Enclosure
.2   Walkdowns of Radiation Monitoring Instrumentation
These reviews represented two inspection samples.  
  a. Inspection Scope
b.  
    The inspectors conducted walkdowns of selected area radiation monitors (ARMs) in the
Findings  
    Unit 1 and Unit 2 auxiliary building to determine if these monitors were located and
No findings of significance were identified.  
    provided measurement capability as described in the FSAR and were optimally
.2  
    positioned relative to the potential sources of radiation they were intended to monitor.
Walkdowns of Radiation Monitoring Instrumentation  
    Walkdowns were conducted of those areas where portable survey instruments were
a.  
    source checked and maintained for radiation protection (RP) staff use to determine if
Inspection Scope  
    those instruments designated ready for use were sufficient in number to support the
The inspectors conducted walkdowns of selected area radiation monitors (ARMs) in the  
    RP program, had current calibration stickers, were operable, and were in adequate
Unit 1 and Unit 2 auxiliary building to determine if these monitors were located and  
    physical condition. Also, the inspectors observed the licensees portable survey
provided measurement capability as described in the FSAR and were optimally  
    instrument calibration units and the radiation sources used for operability checks of
positioned relative to the potential sources of radiation they were intended to monitor.
    various radiation measuring instruments to assess their material condition and discussed
Walkdowns were conducted of those areas where portable survey instruments were  
    their use with RP staff to determine if they were used appropriately. Additionally, the
source checked and maintained for radiation protection (RP) staff use to determine if  
    inspectors observed the use of the instrument calibration units, discussed with the staff
those instruments designated ready for use were sufficient in number to support the  
    calibrator output validation methods, and compared calibrator exposed readings with
RP program, had current calibration stickers, were operable, and were in adequate  
    calculated/expected values. The inspectors evaluated compliance with licensee
physical condition. Also, the inspectors observed the licensees portable survey  
    procedures while RP personnel demonstrated the methods for performing source checks
instrument calibration units and the radiation sources used for operability checks of  
    of portable survey instruments and source checks of personnel contamination and portal
various radiation measuring instruments to assess their material condition and discussed  
    monitors located at the egress to the RCA and the plant protected area.
their use with RP staff to determine if they were used appropriately. Additionally, the  
    These reviews represented one partial inspection sample, which combined with
inspectors observed the use of the instrument calibration units, discussed with the staff  
    Section 2OS3.3 constituted one sample.
calibrator output validation methods, and compared calibrator exposed readings with  
  b. Findings
calculated/expected values. The inspectors evaluated compliance with licensee  
    No findings of significance were identified.
procedures while RP personnel demonstrated the methods for performing source checks  
.3   Calibration and Testing of Radiation Monitoring Instrumentation
of portable survey instruments and source checks of personnel contamination and portal  
  a. Inspection Scope
monitors located at the egress to the RCA and the plant protected area.  
    The inspectors selectively reviewed radiological instrumentation associated with
These reviews represented one partial inspection sample, which combined with  
    monitoring transient high and/or very high radiation areas, instruments used for remote
Section 2OS3.3 constituted one sample.  
    emergency assessment, and radiation monitors used to identify personnel contamination
b.  
    and for assessment of internal exposures to verify that the instruments had been
Findings  
    calibrated as required by the licensees procedures, consistent with industry and
No findings of significance were identified.
    regulatory standards. The inspectors also reviewed alarm setpoints for selected ARMs,
.3  
    for personnel contamination monitors and for portal (egress) monitors to verify that they
Calibration and Testing of Radiation Monitoring Instrumentation  
    were established consistent with the FSAR or TSs, as applicable, and were consistent
a.  
    with industry practices and regulatory guidance. Specifically, the inspectors reviewed
Inspection Scope  
    calibration procedures and the most recent calibration records for the following radiation
The inspectors selectively reviewed radiological instrumentation associated with  
    monitoring instrumentation and calibration equipment:
monitoring transient high and/or very high radiation areas, instruments used for remote  
                                              26                                    Enclosure
emergency assessment, and radiation monitors used to identify personnel contamination  
and for assessment of internal exposures to verify that the instruments had been  
calibrated as required by the licensees procedures, consistent with industry and  
regulatory standards. The inspectors also reviewed alarm setpoints for selected ARMs,  
for personnel contamination monitors and for portal (egress) monitors to verify that they  
were established consistent with the FSAR or TSs, as applicable, and were consistent  
with industry practices and regulatory guidance. Specifically, the inspectors reviewed  
calibration procedures and the most recent calibration records for the following radiation  
monitoring instrumentation and calibration equipment:  


      *       Unit 1 and Unit 2 Containment High Range (Accident) Radiation Monitors;
      *       Unit 1 and Unit 2 Charging Pump Room Low and High Range ARMs;
27
      *       Unit 1 and Unit 2 Seal Table ARMs;
Enclosure
      *       Unit 1 and Unit 2 Post-Accident Sample Line Monitors;
*  
      *       Common Unit Safety Injection Pump Room Low and High Range ARMs;
Unit 1 and Unit 2 Containment High Range (Accident) Radiation Monitors;  
      *       Portable Gamma and Neutron Survey Instruments (Model AMP-100 and ASP-1);
*  
      *       Portable Air Sampler (Model AMS-4);
Unit 1 and Unit 2 Charging Pump Room Low and High Range ARMs;  
      *       Portal (Gamma) Monitors Used at RCA and Protected Area Egresses;
*  
      *       Personnel Contamination Monitors Used at RCA Egress;
Unit 1 and Unit 2 Seal Table ARMs;
      *       Two Instrument Calibrators (and the associated instruments used to measure
*  
              calibrator output); and
Unit 1 and Unit 2 Post-Accident Sample Line Monitors;  
      *       Whole Body Counter.
*  
      The inspectors determined what actions were taken when, during calibration or source
Common Unit Safety Injection Pump Room Low and High Range ARMs;
      checks, an instrument was found significantly out of calibration or exceeded as-found
*  
      acceptance criteria. Should that occur, the inspectors verified that the licensees actions
Portable Gamma and Neutron Survey Instruments (Model AMP-100 and ASP-1);  
      would include a determination of the instruments previous uses and the possible
*  
      consequences of that use since the prior calibration. The inspectors also reviewed the
Portable Air Sampler (Model AMS-4);  
      results of the licensees most recent 10 CFR Part 61 source term (radionuclide mix)
*  
      evaluation to determine if instrument/monitor calibration and check sources were
Portal (Gamma) Monitors Used at RCA and Protected Area Egresses;  
      representative of the plant source term. Given that source term, the inspectors reviewed
*  
      the licensees method for internal dose assessment to determine if difficult to detect
Personnel Contamination Monitors Used at RCA Egress;  
      nuclides were scaled into whole body count dose determinations.
*  
      These reviews represented one partial inspection sample, which combined with
Two Instrument Calibrators (and the associated instruments used to measure  
      Section 2OS3.2 constituted one sample.
calibrator output); and
  b. Findings
*  
      No findings of significance were identified.
Whole Body Counter.  
.4   Problem Identification and Resolution
The inspectors determined what actions were taken when, during calibration or source  
  a. Inspection Scope
checks, an instrument was found significantly out of calibration or exceeded as-found  
      The inspectors reviewed corrective action documents and any special reports that
acceptance criteria. Should that occur, the inspectors verified that the licensees actions  
      involved personnel contamination monitor alarms due to personnel internal exposures to
would include a determination of the instruments previous uses and the possible  
      determine whether identified problems were entered into the corrective action program
consequences of that use since the prior calibration. The inspectors also reviewed the  
      for resolution. Licensee self-assessments, audits, and corrective action documents were
results of the licensees most recent 10 CFR Part 61 source term (radionuclide mix)  
      also reviewed to determine if problems with radiological instrumentation or with self-
evaluation to determine if instrument/monitor calibration and check sources were  
      contained breathing apparatus (SCBA) were identified, characterized, prioritized, and
representative of the plant source term. Given that source term, the inspectors reviewed  
      resolved effectively using the corrective action program.
the licensees method for internal dose assessment to determine if difficult to detect  
      While no internal exposure with a CEDE greater than 50 millirem occurred since the last
nuclides were scaled into whole body count dose determinations.  
      inspection in this area, the inspectors reviewed the licensees methodology for internal
These reviews represented one partial inspection sample, which combined with  
      dose assessment.
Section 2OS3.2 constituted one sample.  
      The inspectors reviewed corrective action program reports related to exposure-
  b. Findings  
      significant radiological incidents that involved radiation monitoring instrument
No findings of significance were identified.  
      deficiencies since the last inspection in this area, as applicable. Members of the RP
.4  
      staff were interviewed and corrective action documents were reviewed to determine
Problem Identification and Resolution  
                                                27                                    Enclosure
a.  
Inspection Scope  
The inspectors reviewed corrective action documents and any special reports that  
involved personnel contamination monitor alarms due to personnel internal exposures to  
determine whether identified problems were entered into the corrective action program  
for resolution. Licensee self-assessments, audits, and corrective action documents were  
also reviewed to determine if problems with radiological instrumentation or with self-
contained breathing apparatus (SCBA) were identified, characterized, prioritized, and  
resolved effectively using the corrective action program.
While no internal exposure with a CEDE greater than 50 millirem occurred since the last  
inspection in this area, the inspectors reviewed the licensees methodology for internal  
dose assessment.  
The inspectors reviewed corrective action program reports related to exposure-
significant radiological incidents that involved radiation monitoring instrument  
deficiencies since the last inspection in this area, as applicable. Members of the RP  
staff were interviewed and corrective action documents were reviewed to determine  


    whether follow-up activities were being conducted in an effective and timely manner
    commensurate with their importance to safety and risk based on the following:
28
    *       Initial problem identification, characterization, and tracking;
Enclosure
    *       Disposition of operability/reportability issues;
whether follow-up activities were being conducted in an effective and timely manner  
    *       Evaluation of safety significance/risk and priority for resolution;
commensurate with their importance to safety and risk based on the following:  
    *       Identification of repetitive problems;
*  
    *       Identification of contributing causes;
Initial problem identification, characterization, and tracking;  
    *       Resolution of Non-Cited Violations tracked in the corrective action program; and
*  
    *       Identification and implementation of effective corrective actions.
Disposition of operability/reportability issues;  
    The inspectors determined if the licensees self-assessment and audit activities
*  
    completed for the approximate two-year period that preceded the inspection were
Evaluation of safety significance/risk and priority for resolution;  
    identifying and addressing repetitive deficiencies or significant individual deficiencies in
*  
    problem identification and resolution, as applicable.
Identification of repetitive problems;  
    These reviews represented three inspection samples.
*  
  b. Findings
Identification of contributing causes;
    No findings of significance were identified.
*  
.5   RP Technician Instrument Use
Resolution of Non-Cited Violations tracked in the corrective action program; and  
  a. Inspection Scope
*  
    The inspectors selectively determined whether calibrations for those survey instruments
Identification and implementation of effective corrective actions.  
    used to perform job coverage surveys and for those currently designated for use had not
The inspectors determined if the licensees self-assessment and audit activities  
    lapsed. The inspectors reviewed instrument issue logs for selected dates in 2007 to
completed for the approximate two-year period that preceded the inspection were  
    determine if response checks of portable survey instruments and checks of instruments
identifying and addressing repetitive deficiencies or significant individual deficiencies in  
    used for unconditional release of materials and workers from the RCA were completed
problem identification and resolution, as applicable.  
    prior to instrument use, or daily, as required by the licensees procedure. The inspectors
These reviews represented three inspection samples.  
    also discussed instrument calibration methods and source response check practices
b.  
    with radiation protection staff and observed staff demonstrate instrument source checks.
Findings  
    These reviews represented one inspection sample.
No findings of significance were identified.  
  b. Findings
.5  
    No findings of significance were identified.
RP Technician Instrument Use  
.6   SCBA Maintenance/Inspection and Emergency Response Staff Qualifications
a.  
  a. Inspection Scope
Inspection Scope  
    The inspectors reviewed aspects of the licensees respiratory protection program for
The inspectors selectively determined whether calibrations for those survey instruments  
    compliance with the requirements of Subpart H of 10 CFR Part 20 and to determine if
used to perform job coverage surveys and for those currently designated for use had not  
    SCBA equipment was properly inspected, maintained, and ready for emergency use.
lapsed. The inspectors reviewed instrument issue logs for selected dates in 2007 to  
    The inspectors reviewed records of inspection and functional tests performed in 2006
determine if response checks of portable survey instruments and checks of instruments  
    and 2007 for all SCBAs staged in the plant to support both the licensees fire brigade
used for unconditional release of materials and workers from the RCA were completed  
    and emergency response organization, as provided in the Point Beach Emergency Plan.
prior to instrument use, or daily, as required by the licensees procedure. The inspectors  
                                                28                                      Enclosure
also discussed instrument calibration methods and source response check practices  
with radiation protection staff and observed staff demonstrate instrument source checks.  
These reviews represented one inspection sample.  
b.  
Findings  
No findings of significance were identified.  
.6  
SCBA Maintenance/Inspection and Emergency Response Staff Qualifications  
a.  
Inspection Scope  
The inspectors reviewed aspects of the licensees respiratory protection program for  
compliance with the requirements of Subpart H of 10 CFR Part 20 and to determine if  
SCBA equipment was properly inspected, maintained, and ready for emergency use.
The inspectors reviewed records of inspection and functional tests performed in 2006  
and 2007 for all SCBAs staged in the plant to support both the licensees fire brigade  
and emergency response organization, as provided in the Point Beach Emergency Plan.  


      The inspectors evaluated the licensees capabilities for refilling and transporting SCBA
      air bottles to and from the control room during emergency conditions. The inspectors
29
      determined if control room staff designated for the active on shift duty roster were
Enclosure
      trained, respirator fit-tested, and medically certified to use SCBAs. Additionally, the
The inspectors evaluated the licensees capabilities for refilling and transporting SCBA  
      inspectors reviewed SCBA qualification records for the licensees radiological
air bottles to and from the control room during emergency conditions. The inspectors  
      emergency teams, including the radiation protection, chemistry, and maintenance staffs,
determined if control room staff designated for the active on shift duty roster were  
      to determine if a sufficient number of staff were qualified to fulfill emergency response
trained, respirator fit-tested, and medically certified to use SCBAs. Additionally, the  
      positions consistent with the Emergency Plan and the requirements of 10 CFR 50.47.
inspectors reviewed SCBA qualification records for the licensees radiological  
      The inspectors also reviewed the respiratory protection training lesson plan to assess its
emergency teams, including the radiation protection, chemistry, and maintenance staffs,  
      overall adequacy relative to Subpart H of 10 CFR Part 20.
to determine if a sufficient number of staff were qualified to fulfill emergency response  
      The inspectors walked down SCBA equipment maintained in the control room, the
positions consistent with the Emergency Plan and the requirements of 10 CFR 50.47.
      Operations Support Center, various areas of the turbine building and in the warehouse
The inspectors also reviewed the respiratory protection training lesson plan to assess its  
      fire brigade ready rooms, as well as spare SCBA air bottle stations. During these
overall adequacy relative to Subpart H of 10 CFR Part 20.  
      walkdowns, the inspectors examined numerous SCBA units to assess their material
The inspectors walked down SCBA equipment maintained in the control room, the  
      condition and to determine if air bottle hydrostatic tests were current and if bottles were
Operations Support Center, various areas of the turbine building and in the warehouse  
      pressurized to meet procedural requirements. The inspectors reviewed records of
fire brigade ready rooms, as well as spare SCBA air bottle stations. During these  
      SCBA equipment inspection and functional testing, including results of the most recent
walkdowns, the inspectors examined numerous SCBA units to assess their material  
      regulator flow tests for all SCBA units maintained at the site. Additionally, the inspectors
condition and to determine if air bottle hydrostatic tests were current and if bottles were  
      observed members of the licensees operations and RP staffs demonstrate the methods
pressurized to meet procedural requirements. The inspectors reviewed records of  
      used to conduct the inspections and functional tests to determine if these activities were
SCBA equipment inspection and functional testing, including results of the most recent  
      performed consistent with procedure and the equipment manufacturers
regulator flow tests for all SCBA units maintained at the site. Additionally, the inspectors  
      recommendations. The inspectors also evaluated through record review and
observed members of the licensees operations and RP staffs demonstrate the methods  
      observations if the required air cylinder hydrostatic testing was documented and current,
used to conduct the inspections and functional tests to determine if these activities were  
      if the Department of Transportation required retest air cylinder markings were in place
performed consistent with procedure and the equipment manufacturers  
      for numerous randomly selected SCBA units and spare air bottles, and if air quality for
recommendations. The inspectors also evaluated through record review and  
      the compressor used to fill SCBA air bottles was routinely tested to verify Grade-D
observations if the required air cylinder hydrostatic testing was documented and current,  
      quality. The inspectors also reviewed the qualification documentation (training
if the Department of Transportation required retest air cylinder markings were in place  
      certificate) issued by the SCBA manufacturer to an individual contracted by the licensee
for numerous randomly selected SCBA units and spare air bottles, and if air quality for  
      to perform maintenance/repair of SCBA vital components. Pressure regulator test/repair
the compressor used to fill SCBA air bottles was routinely tested to verify Grade-D  
      records for 2007 for all SCBA units designated for emergency use were reviewed to
quality. The inspectors also reviewed the qualification documentation (training  
      determine if the equipment was adequately maintained consistent with the
certificate) issued by the SCBA manufacturer to an individual contracted by the licensee  
      manufacturers maintenance procedure.
to perform maintenance/repair of SCBA vital components. Pressure regulator test/repair  
      These reviews represented two inspection samples.
records for 2007 for all SCBA units designated for emergency use were reviewed to  
  b. Findings
determine if the equipment was adequately maintained consistent with the  
      No findings of significance were identified.
manufacturers maintenance procedure.
4.   OTHER ACTIVITIES
These reviews represented two inspection samples.  
4OA1 Performance Indicator (PI) Verification (71151)
b.  
.1   Data Submission Issue
Findings  
  a. Inspection Scope
No findings of significance were identified.  
      The inspectors performed a review of the data submitted by the licensee for the 4th
4.  
      quarter 2007 PIs for any obvious inconsistencies prior to its public release in accordance
OTHER ACTIVITIES  
      with IMC 0608, Performance Indicator Program.
4OA1 Performance Indicator (PI) Verification (71151)  
                                                29                                        Enclosure
.1  
Data Submission Issue
a.  
Inspection Scope  
The inspectors performed a review of the data submitted by the licensee for the 4th  
quarter 2007 PIs for any obvious inconsistencies prior to its public release in accordance  
with IMC 0608, Performance Indicator Program.  


    This review was performed as part of the inspectors normal plant status activities and,
    as such, did not constitute a separate inspection sample.
30
  b. Findings
Enclosure
    No findings of significance were identified.
This review was performed as part of the inspectors normal plant status activities and,  
.2   Mitigating Systems Performance Index - Emergency AC Power System
as such, did not constitute a separate inspection sample.  
  a. Inspection Scope
b.  
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
Findings  
    Index (MSPI) Emergency AC Power System PIs, for both Units, for July 2006 through
No findings of significance were identified.  
    March 2007. To determine the accuracy of the data the inspectors used definitions and
.2  
    guidance in Revision 5 of the Nuclear Energy Institute (NEI) Document 99-02,
Mitigating Systems Performance Index - Emergency AC Power System  
    Regulatory Assessment Performance Indicator Guideline. The inspectors reviewed the
a.  
    licensees operator narrative logs, MSPI derivation reports, issue reports, event reports,
Inspection Scope  
    and NRC integrated inspection reports for July 1, 2006, to March 31, 2007, to validate
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
    the accuracy of the submittals. The inspectors reviewed the MSPI component risk
Index (MSPI) Emergency AC Power System PIs, for both Units, for July 2006 through  
    coefficient to determine if it had changed by more than 25 percent since the previous
March 2007. To determine the accuracy of the data the inspectors used definitions and  
    inspection, and if so, that the change was in accordance with applicable NEI guidance.
guidance in Revision 5 of the Nuclear Energy Institute (NEI) Document 99-02,  
    The inspectors also reviewed the licensees issue report database to determine if any
Regulatory Assessment Performance Indicator Guideline. The inspectors reviewed the  
    problems had been identified with the PI data collected or transmitted for this indicator;
licensees operator narrative logs, MSPI derivation reports, issue reports, event reports,  
    were identified.
and NRC integrated inspection reports for July 1, 2006, to March 31, 2007, to validate  
    This inspection constituted two MSPI emergency AC power system samples.
the accuracy of the submittals. The inspectors reviewed the MSPI component risk  
  b. Findings
coefficient to determine if it had changed by more than 25 percent since the previous  
    No findings of significance were identified.
inspection, and if so, that the change was in accordance with applicable NEI guidance.
.3   Mitigating Systems Performance Index - High Pressure Injection Systems
The inspectors also reviewed the licensees issue report database to determine if any  
  a. Inspection Scope
problems had been identified with the PI data collected or transmitted for this indicator;  
    The inspectors sampled licensee submittals for the MSPI - High Pressure Injection
were identified.  
    Systems PIs, for both Units, for July 2006 through March 2007. To determine the
This inspection constituted two MSPI emergency AC power system samples.  
    accuracy of the PI data the inspectors used definitions and guidance contained in
b.  
    NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue
Findings  
    reports, MSPI derivation reports, event reports, and NRC integrated inspection reports
No findings of significance were identified.  
    for July 1, 2006 to March 31, 2007, to validate the accuracy of the submittals. The
.3  
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
Mitigating Systems Performance Index - High Pressure Injection Systems  
    by more than 25 percent since the previous inspection, and if so, that the change was in
a.  
    accordance with applicable NEI guidance. The inspectors also reviewed the licensees
Inspection Scope  
    issue report database to determine if any problems had been identified with the PI data
The inspectors sampled licensee submittals for the MSPI - High Pressure Injection  
    collected or transmitted for this indicator and none were identified.
Systems PIs, for both Units, for July 2006 through March 2007. To determine the  
    This inspection constituted two MSPI high pressure injection system samples.
accuracy of the PI data the inspectors used definitions and guidance contained in      
                                              30                                      Enclosure
NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue  
reports, MSPI derivation reports, event reports, and NRC integrated inspection reports  
for July 1, 2006 to March 31, 2007, to validate the accuracy of the submittals. The  
inspectors reviewed the MSPI component risk coefficient to determine if it had changed  
by more than 25 percent since the previous inspection, and if so, that the change was in  
accordance with applicable NEI guidance. The inspectors also reviewed the licensees  
issue report database to determine if any problems had been identified with the PI data  
collected or transmitted for this indicator and none were identified.  
This inspection constituted two MSPI high pressure injection system samples.  


  b. Findings
    No findings of significance were identified.
31
.4   Mitigating Systems Performance Index - Heat Removal System
Enclosure
  a. Inspection Scope
b.  
    The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI, for
Findings  
    both Units, for July 2006 through March 2007. To determine the accuracy of the PI data
No findings of significance were identified.  
    reported during that period, the inspectors used PI definitions and guidance in
.4  
    NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue
Mitigating Systems Performance Index - Heat Removal System  
    reports, event reports, MSPI derivation reports, and NRC integrated inspection reports
a.  
    for July 1, 2006, to March 31, 2007, to validate the accuracy of the submittals. The
Inspection Scope  
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI, for  
    by more than 25 percent since the previous inspection, and if so, that the change was in
both Units, for July 2006 through March 2007. To determine the accuracy of the PI data  
    accordance with applicable NEI guidance. The inspectors also reviewed the licensees
reported during that period, the inspectors used PI definitions and guidance in  
    issue report database to determine if any problems had been identified with the PI data
NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue  
    collected or transmitted for this indicator and none were identified.
reports, event reports, MSPI derivation reports, and NRC integrated inspection reports  
    This inspection constituted two MSPI heat removal system samples.
for July 1, 2006, to March 31, 2007, to validate the accuracy of the submittals. The  
  b. Findings
inspectors reviewed the MSPI component risk coefficient to determine if it had changed  
    No findings of significance were identified.
by more than 25 percent since the previous inspection, and if so, that the change was in  
.5   Mitigating Systems Performance Index - Residual Heat Removal System
accordance with applicable NEI guidance. The inspectors also reviewed the licensees  
  a. Inspection Scope
issue report database to determine if any problems had been identified with the PI data  
    The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal
collected or transmitted for this indicator and none were identified.  
    System PI, for both Units, for July 2006 through March 2007. To determine the accuracy
This inspection constituted two MSPI heat removal system samples.  
    of the PI data reported during that period the inspectors used definitions and guidance in
b.  
    NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue
Findings  
    reports, MSPI derivation reports, event reports, and NRC integrated inspection reports
No findings of significance were identified.  
    for July 1, 2006, to March 31, 2007, to validate the accuracy of the submittals. The
.5  
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
Mitigating Systems Performance Index - Residual Heat Removal System  
    by more than 25 percent in value since the previous inspection, and if so, that the
a.  
    change was in accordance with applicable NEI guidance. The inspectors also reviewed
Inspection Scope  
    the licensees issue report database to determine if any problems had been identified
The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal  
    with the PI data collected or transmitted for this indicator and none were identified.
System PI, for both Units, for July 2006 through March 2007. To determine the accuracy  
    This inspection constituted two MSPI residual heat removal system samples.
of the PI data reported during that period the inspectors used definitions and guidance in  
  b. Findings
NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue  
    No findings of significance were identified.
reports, MSPI derivation reports, event reports, and NRC integrated inspection reports  
                                              31                                      Enclosure
for July 1, 2006, to March 31, 2007, to validate the accuracy of the submittals. The  
inspectors reviewed the MSPI component risk coefficient to determine if it had changed  
by more than 25 percent in value since the previous inspection, and if so, that the  
change was in accordance with applicable NEI guidance. The inspectors also reviewed  
the licensees issue report database to determine if any problems had been identified  
with the PI data collected or transmitted for this indicator and none were identified.  
This inspection constituted two MSPI residual heat removal system samples.  
b.  
Findings  
No findings of significance were identified.  


.6   Mitigating Systems Performance Index - Cooling Water Systems
  a. Inspection Scope
32
      The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems PI for
Enclosure
      July 2006 through March 2007. To determine the accuracy of the PI data reported
.6  
      during those periods, the inspectors used definitions and guidance in NEI 99-02. The
Mitigating Systems Performance Index - Cooling Water Systems  
      inspectors reviewed the licensees operator narrative logs, issue reports, MSPI
a.  
      derivation reports, event reports, and NRC integrated inspection reports for July 1, 2006,
Inspection Scope  
      to March 31, 2007, to validate the accuracy of the submittals. The inspectors reviewed
The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems PI for  
      the MSPI component risk coefficient to determine if it had changed by more than
July 2006 through March 2007. To determine the accuracy of the PI data reported  
      25 percent since the previous inspection, and if so, that the change was in accordance
during those periods, the inspectors used definitions and guidance in NEI 99-02. The  
      with applicable NEI guidance. The inspectors also reviewed the licensees issue report
inspectors reviewed the licensees operator narrative logs, issue reports, MSPI  
      database to determine if any problems had been identified with the PI data collected or
derivation reports, event reports, and NRC integrated inspection reports for July 1, 2006,  
      transmitted for this indicator and none were identified.
to March 31, 2007, to validate the accuracy of the submittals. The inspectors reviewed  
      This inspection constituted two MSPI cooling water system samples.
the MSPI component risk coefficient to determine if it had changed by more than  
  b. Findings
25 percent since the previous inspection, and if so, that the change was in accordance  
      No findings of significance were identified.
with applicable NEI guidance. The inspectors also reviewed the licensees issue report  
.7   Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent
database to determine if any problems had been identified with the PI data collected or  
      Occurrences
transmitted for this indicator and none were identified.  
  a. Inspection Scope
This inspection constituted two MSPI cooling water system samples.  
      The inspectors used definitions and guidance contained in Revision 5 of NEI 99-02
b.  
      to verify the accuracy of the data for the Radiological Effluent Technical
Findings  
      Specification/Offsite Dose Calculation Manual (RETS/ODCM) Radiological Effluent
No findings of significance were identified.  
      Occurrence PI.
.7  
      The inspectors reviewed the licensees CAP database and selected individual condition
Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent  
      reports generated between December 2006 and November 2007 to identify any potential
Occurrences  
      occurrences such as unmonitored, uncontrolled, or improperly calculated effluent
a.  
      releases that may have impacted offsite dose. The inspectors also selectively reviewed
Inspection Scope  
      gaseous and liquid effluent summary data and the results of associated offsite dose
The inspectors used definitions and guidance contained in Revision 5 of NEI 99-02  
      calculations for selected periods in 2007 to determine if indicator results were accurately
to verify the accuracy of the data for the Radiological Effluent Technical  
      reported. The inspectors also discussed with the licensee the methods for quantifying
Specification/Offsite Dose Calculation Manual (RETS/ODCM) Radiological Effluent  
      gaseous and liquid effluents and for determining effluent dose.
Occurrence PI.  
      These reviews represented one inspection sample.
The inspectors reviewed the licensees CAP database and selected individual condition  
  b. Findings
reports generated between December 2006 and November 2007 to identify any potential  
      No findings of significance were identified.
occurrences such as unmonitored, uncontrolled, or improperly calculated effluent  
                                                32                                      Enclosure
releases that may have impacted offsite dose. The inspectors also selectively reviewed  
gaseous and liquid effluent summary data and the results of associated offsite dose  
calculations for selected periods in 2007 to determine if indicator results were accurately  
reported. The inspectors also discussed with the licensee the methods for quantifying  
gaseous and liquid effluents and for determining effluent dose.
These reviews represented one inspection sample.  
  b. Findings  
No findings of significance were identified.  


4OA2 Problem Identification and Resolution (71152)
  .1   Routine Resident Inspector Review
33
  a. Inspection Scope
Enclosure
      As discussed in previous sections of this report, the inspectors routinely reviewed
4OA2 Problem Identification and Resolution (71152)  
      issues during baseline inspection activities and plant status reviews to determine
.1  
      whether issues were entered into the licensees corrective action program at an
Routine Resident Inspector Review  
      appropriate threshold, that adequate attention was given to timely corrective actions, and
a.  
      that adverse trends were identified and addressed. The inspectors also reviewed all
Inspection Scope  
      CAPs written during the inspection period. The CAPs written by the licensee as a result
As discussed in previous sections of this report, the inspectors routinely reviewed  
      of inspectors observations are included in the list of documents in the Attachment to this
issues during baseline inspection activities and plant status reviews to determine  
      report.
whether issues were entered into the licensees corrective action program at an  
  b. Findings
appropriate threshold, that adequate attention was given to timely corrective actions, and  
      No findings of significance were identified.
that adverse trends were identified and addressed. The inspectors also reviewed all  
.2   Selected Issue Follow-up Inspection: Annual Review of Operator Workarounds
CAPs written during the inspection period. The CAPs written by the licensee as a result  
      Introduction
of inspectors observations are included in the list of documents in the Attachment to this  
      The inspectors selected operator workarounds for a more in-depth review in accordance
report.  
      with Inspection Procedure requirements.
b.  
      This annual review of operator workarounds constituted one inspection sample.
Findings  
  a. Effectiveness of Problem Identification
No findings of significance were identified.  
  (1) Inspection Scope
.2  
      The inspectors reviewed plant logs, condition reports, and work requests to verify that
Selected Issue Follow-up Inspection: Annual Review of Operator Workarounds  
      the licensees identification of operator workarounds was complete, accurate, and timely,
Introduction  
      and that the consideration of extent of condition review, generic implications, common
The inspectors selected operator workarounds for a more in-depth review in accordance  
      cause, and previous occurrences was adequate.
with Inspection Procedure requirements.  
  (2) Findings and Issues
This annual review of operator workarounds constituted one inspection sample.  
      No findings of significance were identified. No issues were identified.
a.  
  b. Prioritization and Evaluation of Issues
Effectiveness of Problem Identification  
  (1) Inspection Scope
(1) Inspection Scope  
      The inspectors reviewed plant logs, condition reports, and work requests associated with
The inspectors reviewed plant logs, condition reports, and work requests to verify that  
      existing operator burdens, including operator workarounds, operator challenges, and
the licensees identification of operator workarounds was complete, accurate, and timely,  
      control room deficiencies. The nature and significance of individual issues and all issues
and that the consideration of extent of condition review, generic implications, common  
      in aggregate with respect to safety, risk, and licensee corrective action procedural
cause, and previous occurrences was adequate.  
      requirements were considered. Additionally, the inspectors assessed the licensees
(2) Findings and Issues  
      evaluation and disposition of performance issues, evaluation and disposition of
No findings of significance were identified. No issues were identified.  
      operability issues, and application of risk insights for prioritization of issues.
b.  
                                                33                                      Enclosure
Prioritization and Evaluation of Issues  
(1) Inspection Scope  
The inspectors reviewed plant logs, condition reports, and work requests associated with  
existing operator burdens, including operator workarounds, operator challenges, and  
control room deficiencies. The nature and significance of individual issues and all issues  
in aggregate with respect to safety, risk, and licensee corrective action procedural  
requirements were considered. Additionally, the inspectors assessed the licensees  
evaluation and disposition of performance issues, evaluation and disposition of  
operability issues, and application of risk insights for prioritization of issues.  


  (2) Findings and Issues
      No findings of significance were identified. No issues were identified.
34
  c. Effectiveness of Corrective Actions
Enclosure
  (1) Inspection Scope
(2) Findings and Issues  
      The inspectors reviewed condition reports and work requests associated with existing
No findings of significance were identified. No issues were identified.  
      operator workarounds, operator challenges, and control room deficiencies to determine if
c.  
      the licensees corrective action program addressed generic implications. Additionally,
Effectiveness of Corrective Actions  
      the inspectors verified that established corrective actions by the licensee were
(1) Inspection Scope  
      appropriately focused to correct the problem.
The inspectors reviewed condition reports and work requests associated with existing  
  (2) Findings and Issues
operator workarounds, operator challenges, and control room deficiencies to determine if  
      No findings of significance were identified. No issues were identified.
the licensees corrective action program addressed generic implications. Additionally,  
.3   Semiannual Trend Review
the inspectors verified that established corrective actions by the licensee were  
  a. Inspection Scope
appropriately focused to correct the problem.  
      The inspectors reviewed of the licensees CAPs and associated documents to identify
(2) Findings and Issues  
      trends that could indicate the existence of a more significant safety issue. The
No findings of significance were identified. No issues were identified.  
      inspectors review was focused on repetitive equipment issues, but also considered the
.3  
      results of daily inspector CAP item screening discussed in Section 4OA2 above,
Semiannual Trend Review  
      licensee trending efforts, and licensee human performance results. The inspectors
a.  
      review nominally considered July 2007 through December 2007, although some
Inspection Scope  
      examples expanded beyond those dates.
The inspectors reviewed of the licensees CAPs and associated documents to identify  
      The reviews also included issues documented outside the normal corrective action
trends that could indicate the existence of a more significant safety issue. The  
      program in major equipment problem lists, repetitive and/or rework maintenance lists,
inspectors review was focused on repetitive equipment issues, but also considered the  
      departmental problem/challenges lists, system health reports, quality assurance
results of daily inspector CAP item screening discussed in Section 4OA2 above,  
      audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.
licensee trending efforts, and licensee human performance results. The inspectors  
      The inspectors compared and contrasted their results with the results contained in the
review nominally considered July 2007 through December 2007, although some  
      licensees corrective action program trending reports. Corrective actions associated with
examples expanded beyond those dates.
      a sample of the issues identified in the licensees trending reports were reviewed for
The reviews also included issues documented outside the normal corrective action  
      adequacy.
program in major equipment problem lists, repetitive and/or rework maintenance lists,  
      This semi-annual trend review by the inspectors constituted one inspection.
departmental problem/challenges lists, system health reports, quality assurance  
  b. Findings and Issues.
audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.
      No findings of significance were identified. No issues were identified.
The inspectors compared and contrasted their results with the results contained in the  
                                                34                                    Enclosure
licensees corrective action program trending reports. Corrective actions associated with  
a sample of the issues identified in the licensees trending reports were reviewed for  
adequacy.  
This semi-annual trend review by the inspectors constituted one inspection.  
b.  
Findings and Issues.  
No findings of significance were identified. No issues were identified.  


4OA3 Followup of Events and Notices of Enforcement Discretion (71153)
.1   TS-Required Shutdown Due to High Unit 2 Refueling Water Storage Tank Temperature
35
  a. Inspection Scope
Enclosure
      Through record reviews and discussion with plant staff, the inspectors assessed the
4OA3 Followup of Events and Notices of Enforcement Discretion (71153)  
      circumstances of a TS-required shutdown initiated on September 18, 2007. Although
.1  
      the licensee took immediate corrective actions to de-energize the submersion heaters
TS-Required Shutdown Due to High Unit 2 Refueling Water Storage Tank Temperature  
      and cool the RWST by forced recirculation, the temperature could not be restored to
a.  
      acceptable limits before the eight-hour TS action statement expired. As a result, Unit 2
Inspection Scope  
      commenced a TS-required shutdown that was later averted, while at approximately
Through record reviews and discussion with plant staff, the inspectors assessed the  
      20 percent reactor power, when the RWST temperature was restored to within
circumstances of a TS-required shutdown initiated on September 18, 2007. Although  
      acceptable limits. The inspection scope included a review of the events leading up to
the licensee took immediate corrective actions to de-energize the submersion heaters  
      the shutdown initiation.
and cool the RWST by forced recirculation, the temperature could not be restored to  
  b. Findings
acceptable limits before the eight-hour TS action statement expired. As a result, Unit 2  
      Introduction: A self-revealing finding of very low safety significance (Green) and an
commenced a TS-required shutdown that was later averted, while at approximately  
      associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion V,
20 percent reactor power, when the RWST temperature was restored to within  
      Instructions, Procedures, and Drawings, was identified for the failure to allow operators
acceptable limits. The inspection scope included a review of the events leading up to  
      to properly set the thermostat of the Unit 2 RWST heaters, and to ensure that the RWST
the shutdown initiation.
      was recirculated frequently enough for the temperature indicator to accurately measure
      bulk temperature.
b. Findings  
      Description: On September 18, 2007, during the performance of TS-required
Introduction: A self-revealing finding of very low safety significance (Green) and an  
      surveillance SR 3.5.4.1, the Unit 2 RWST was found to be at 105 °F. The TS
associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion V,  
      maximum allowable limit was 100 °F (97 °F parametric). Because RWST temperature
Instructions, Procedures, and Drawings, was identified for the failure to allow operators  
      could not be restored within the allowed eight hours, operators commenced a shutdown
to properly set the thermostat of the Unit 2 RWST heaters, and to ensure that the RWST  
      of Unit 2. At 20 percent power, the temperature was returned to within acceptable limits
was recirculated frequently enough for the temperature indicator to accurately measure  
      and the operators began to raise reactor power to 100 percent. The cause of the
bulk temperature.  
      elevated temperature was found to be the incorrectly set RWST heater thermostat.
Description: On September 18, 2007, during the performance of TS-required  
      It was identified that on August 30, the controlling thermostat for the RWST heaters was
surveillance SR 3.5.4.1, the Unit 2 RWST was found to be at 105 °F. The TS  
      incorrectly set to 95 °F vice 50 °F as required by procedure. For the 18 days between
maximum allowable limit was 100 °F (97 °F parametric). Because RWST temperature  
      August 30 and September 18, the bulk water temperature increased to 105 °F through
could not be restored within the allowed eight hours, operators commenced a shutdown  
      natural circulation. During this period, daily temperature readings of the RWST only
of Unit 2. At 20 percent power, the temperature was returned to within acceptable limits  
      showed an increase from 75 °F to 85 °F. This disparity occurred due to stratification
and the operators began to raise reactor power to 100 percent. The cause of the  
      caused by the location of the single temperature indicator relative to the heaters inside
elevated temperature was found to be the incorrectly set RWST heater thermostat.  
      the tank. Because the RWST temperature indicator is located 2 feet from the bottom of
It was identified that on August 30, the controlling thermostat for the RWST heaters was  
      the 70 foot tall tank, and the heaters are located 4.5 feet above the indicator,
incorrectly set to 95 °F vice 50 °F as required by procedure. For the 18 days between  
      stratification caused the temperature indicator to remain in a layer of colder water. It
August 30 and September 18, the bulk water temperature increased to 105 °F through  
      was not until September 18, that the RWST temperature was found to be at 105 °F, after
natural circulation. During this period, daily temperature readings of the RWST only  
      four hours of being on forced recirculation.
showed an increase from 75 °F to 85 °F. This disparity occurred due to stratification  
      The inspectors reviewed procedure PC 49, part 4, Revision 19, which was used for
caused by the location of the single temperature indicator relative to the heaters inside  
      setting the thermostat on the RWSTs to 50 °F. This task was performed once a year
the tank. Because the RWST temperature indicator is located 2 feet from the bottom of  
      during cold weather preparations to ensure that the RWST remained within the required
the 70 foot tall tank, and the heaters are located 4.5 feet above the indicator,  
      temperature range of 40 to 100 °F. Through this review, the inspectors concluded that a
stratification caused the temperature indicator to remain in a layer of colder water. It  
      lack of sufficient detail existed for the critical step of setting the thermostat, which directly
was not until September 18, that the RWST temperature was found to be at 105 °F, after  
      affected the operability of the safety-related RWST. Specifically, the lack of procedural
four hours of being on forced recirculation.    
                                                  35                                        Enclosure
The inspectors reviewed procedure PC 49, part 4, Revision 19, which was used for  
setting the thermostat on the RWSTs to 50 °F. This task was performed once a year  
during cold weather preparations to ensure that the RWST remained within the required  
temperature range of 40 to 100 °F. Through this review, the inspectors concluded that a  
lack of sufficient detail existed for the critical step of setting the thermostat, which directly  
affected the operability of the safety-related RWST. Specifically, the lack of procedural  


detail contributed to the operators reliance upon an unapproved operator aid in the field;
in this case, a black marking that was believed by the operator to indicate the desired
36
thermostat setting.
Enclosure
The inspectors also reviewed procedure PC 25, Revision 23, which was used to
detail contributed to the operators reliance upon an unapproved operator aid in the field;  
recirculate and purify the RWST. This task was performed to keep the RWST contents
in this case, a black marking that was believed by the operator to indicate the desired  
in a homogeneous mixture to prevent stratification. Through this review, the inspectors
thermostat setting.  
concluded that the frequency of RWST recirculation, which was performed monthly, was
The inspectors also reviewed procedure PC 25, Revision 23, which was used to  
inadequate to ensure that the temperature indicator accurately read bulk tank
recirculate and purify the RWST. This task was performed to keep the RWST contents  
temperature to satisfy the TS operability requirements, while the heaters were
in a homogeneous mixture to prevent stratification. Through this review, the inspectors  
energized.
concluded that the frequency of RWST recirculation, which was performed monthly, was  
Analysis: The inspectors determined that the failure to have adequate procedures in
inadequate to ensure that the temperature indicator accurately read bulk tank  
place to ensure the operability of the safety related RWST is a performance deficiency
temperature to satisfy the TS operability requirements, while the heaters were  
and a finding. The finding is more than minor in accordance with IMC 0612, Power
energized.  
Reactor Inspection Reports, Appendix B, Issue Screening, dated September 20, 2007,
Analysis: The inspectors determined that the failure to have adequate procedures in  
because it is associated with the procedural quality and human performance attributes of
place to ensure the operability of the safety related RWST is a performance deficiency  
the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring
and a finding. The finding is more than minor in accordance with IMC 0612, Power  
the availability, reliability, and capability of systems that respond to initiating events to
Reactor Inspection Reports, Appendix B, Issue Screening, dated September 20, 2007,  
prevent undesirable consequences.
because it is associated with the procedural quality and human performance attributes of  
Using IMC 0609, Significance Determination Process, dated January 10, 2008, the
the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring  
inspectors determined that the finding is of very low safety significance (Green) because
the availability, reliability, and capability of systems that respond to initiating events to  
the finding did not involve a design deficiency, there was no actual loss of safety
prevent undesirable consequences.  
function, no single train loss of safety function for greater than the TS allowed outage
Using IMC 0609, Significance Determination Process, dated January 10, 2008, the  
time, and no risk due to external events. The inspectors also determined that the finding
inspectors determined that the finding is of very low safety significance (Green) because  
had a cross-cutting aspect in the area of human performance. Specifically, human error
the finding did not involve a design deficiency, there was no actual loss of safety  
prevention techniques were not utilized prior to and during the thermostat setting task
function, no single train loss of safety function for greater than the TS allowed outage  
and personnel proceeded in the face of uncertainty and unexpected circumstances
time, and no risk due to external events. The inspectors also determined that the finding  
(H.4(a)).
had a cross-cutting aspect in the area of human performance. Specifically, human error  
Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and
prevention techniques were not utilized prior to and during the thermostat setting task  
Drawings, requires, in part, that activities affecting quality be prescribed by documented
and personnel proceeded in the face of uncertainty and unexpected circumstances  
instructions, procedures, or drawings, of a type appropriate to the circumstances and
(H.4(a)).  
shall be accomplished in accordance with these instructions, procedures and drawings.
Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and  
Contrary to this, the licensees procedure PC 49, part 4, used for setting the RWST
Drawings, requires, in part, that activities affecting quality be prescribed by documented  
heater thermostat, did not have adequate instructions for correctly setting the
instructions, procedures, or drawings, of a type appropriate to the circumstances and  
thermostat. Further, the monthly recirculation of the RWST, specified in procedure
shall be accomplished in accordance with these instructions, procedures and drawings.
PC-25, was not appropriate to ensure that the TS-required temperature readings were
Contrary to this, the licensees procedure PC 49, part 4, used for setting the RWST  
valid in their indication of bulk tank temperature while heaters were energized. Because
heater thermostat, did not have adequate instructions for correctly setting the  
of the very low safety significance of this finding and because the finding was entered
thermostat. Further, the monthly recirculation of the RWST, specified in procedure  
into the licensees corrective action program (CAP 01111841), the violation is being
PC-25, was not appropriate to ensure that the TS-required temperature readings were  
treated as an NCV, consistent with Section VI.A.1 of NRC Enforcement Policy
valid in their indication of bulk tank temperature while heaters were energized. Because  
(NCV 05000266/2007005-04; 05000301/2007005-04).
of the very low safety significance of this finding and because the finding was entered  
The licensee entered the event into its corrective unit action program, took corrective
into the licensees corrective action program (CAP 01111841), the violation is being  
actions to increase the frequency of the Unit 1 and Unit 2 RWST recirculation to once
treated as an NCV, consistent with Section VI.A.1 of NRC Enforcement Policy  
every seven days until the heaters were no longer needed due to seasonal temperature
(NCV 05000266/2007005-04; 05000301/2007005-04).  
increases, and conducted a root cause evaluation.
The licensee entered the event into its corrective unit action program, took corrective  
                                            36                                      Enclosure
actions to increase the frequency of the Unit 1 and Unit 2 RWST recirculation to once  
every seven days until the heaters were no longer needed due to seasonal temperature  
increases, and conducted a root cause evaluation.  


  .2 (Closed) Violation (VIO) 05000266/2006011-01; 050000301/2006011-01: Failure to
    Update Final Safety Analysis Report with Reactor Head Drop Analysis and Obtain NRC
37
    Approval
Enclosure
    The inspectors evaluated the licensees corrective action program responses to the
.2  
    January 29, 2007, Notice of Violation associated with the NRC Special Inspection Report
(Closed) Violation (VIO) 05000266/2006011-01; 050000301/2006011-01: Failure to  
    05000266/2006011; 05000301/2006011, for issues in the spring of 2005, regarding a
Update Final Safety Analysis Report with Reactor Head Drop Analysis and Obtain NRC  
    1982 reactor vessel head drop analysis. The inspectors reviewed the corrective actions
Approval  
    the licensee described in its correspondence dated December 19, 2006, entitled,
The inspectors evaluated the licensees corrective action program responses to the  
    Response to an Apparent Violation in Inspection Report05000266/2006011;
January 29, 2007, Notice of Violation associated with the NRC Special Inspection Report  
    05000301/2006011; EA-06-274. The inspectors validated the following corrective
05000266/2006011; 05000301/2006011, for issues in the spring of 2005, regarding a  
    actions were complete: incorporation of the Reactor Vessel Head Drop Analyses into
1982 reactor vessel head drop analysis. The inspectors reviewed the corrective actions  
    the FSAR; revision of the Technical Requirements Manual Section 3.9.4; revision of
the licensee described in its correspondence dated December 19, 2006, entitled,  
    plant procedures, including maintenance, outage, and operations procedures and
Response to an Apparent Violation in Inspection Report05000266/2006011;  
    checklists; development of a licensing basis policy and training for plant staff on that
05000301/2006011; EA-06-274. The inspectors validated the following corrective  
    policy; development and implementation of a continuing training module for plant
actions were complete: incorporation of the Reactor Vessel Head Drop Analyses into  
    engineers; licensee evaluation and validation of commitments contained in an
the FSAR; revision of the Technical Requirements Manual Section 3.9.4; revision of  
    October 1996 NRC, Request for Information Pursuant to 10 CFR 50.54(f) Regarding
plant procedures, including maintenance, outage, and operations procedures and  
    Adequacy and Availability of Design Basis Information, with corresponding corrective
checklists; development of a licensing basis policy and training for plant staff on that  
    actions for identified deficiencies; and development of a procedure writer/reviewer
policy; development and implementation of a continuing training module for plant  
    certification matrix with a job familiarization guide which addressed how to search the
engineers; licensee evaluation and validation of commitments contained in an  
    sites regulatory information system. The review by the inspectors constituted one
October 1996 NRC, Request for Information Pursuant to 10 CFR 50.54(f) Regarding  
    inspection procedure sample.
Adequacy and Availability of Design Basis Information, with corresponding corrective  
4OA5 Other Activities
actions for identified deficiencies; and development of a procedure writer/reviewer  
.1   (Closed) Unresolved Item (URI) 05000266/2007008-06: Inadequate Post-Maintenance
certification matrix with a job familiarization guide which addressed how to search the  
    Testing (PMT) of the Turbine-Driven Auxiliary Feedwater Pumps Following Major
sites regulatory information system. The review by the inspectors constituted one  
    Maintenance
inspection procedure sample.  
    Introduction: The inspectors identified a finding of very low safety significance (Green)
4OA5 Other Activities  
    and an associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,
.1  
    Instructions, Procedures, and Drawings, for the licensees failure to conduct adequate
(Closed) Unresolved Item (URI) 05000266/2007008-06: Inadequate Post-Maintenance
    PMT of the Unit 1 1P-29 TDAFW pump following a ten-year overhaul of the turbine in
Testing (PMT) of the Turbine-Driven Auxiliary Feedwater Pumps Following Major  
    May 2007. Specifically, the ten-year overhaul maintenance included bearing
Maintenance  
    replacement, but, the PMT did not run the TDAFW pump long enough for bearing
Introduction: The inspectors identified a finding of very low safety significance (Green)  
    temperature to stabilize. The appropriate PMT would have detected that the bearing
and an associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,  
    temperatures were rising and required evaluation prior to declaring the TDAFW
Instructions, Procedures, and Drawings, for the licensees failure to conduct adequate  
    operable.
PMT of the Unit 1 1P-29 TDAFW pump following a ten-year overhaul of the turbine in  
    Description: The licensee completed an overhaul of the Unit 1 TDAFW turbine and the
May 2007. Specifically, the ten-year overhaul maintenance included bearing  
    associated PMT on May 6, 2007, declaring the TDAFW pump operable following
replacement, but, the PMT did not run the TDAFW pump long enough for bearing  
    completion of quarterly IST procedure IT-8A. The PMT requirements for the overhaul
temperature to stabilize. The appropriate PMT would have detected that the bearing  
    were listed in the maintenance overhaul procedure, RMP 9044-1. The IST procedure
temperatures were rising and required evaluation prior to declaring the TDAFW  
    had no specific requirements to monitor bearing temperatures for stabilization other than
operable.  
    to perform the IST, which recorded bearing temperature data. The procedure did have a
Description: The licensee completed an overhaul of the Unit 1 TDAFW turbine and the  
    temperature limit to place the pump in the alert range and conduct an engineering
associated PMT on May 6, 2007, declaring the TDAFW pump operable following  
    evaluation when the turbine outboard bearing exceeded 225 °F, and to remove the
completion of quarterly IST procedure IT-8A. The PMT requirements for the overhaul  
    pump from service and declare the pump inoperable when the same bearing exceeded
were listed in the maintenance overhaul procedure, RMP 9044-1. The IST procedure  
    250 °F. However, as part of the PMT for the ten-year overhaul, there was no
had no specific requirements to monitor bearing temperatures for stabilization other than  
                                                37                                    Enclosure
to perform the IST, which recorded bearing temperature data. The procedure did have a  
temperature limit to place the pump in the alert range and conduct an engineering  
evaluation when the turbine outboard bearing exceeded 225 °F, and to remove the  
pump from service and declare the pump inoperable when the same bearing exceeded  
250 °F. However, as part of the PMT for the ten-year overhaul, there was no  


requirement in either the work order, maintenance procedure or the IST procedure, to
ensure bearing temperatures were stabilized.
38
For testing on May 1, the inspectors noted that the outboard bearing temperature
Enclosure
reached 247 °F, as indicated on the chart recorders. During the PMT on May 6, some
requirement in either the work order, maintenance procedure or the IST procedure, to  
licensee personnel noted the turbine outboard bearing rising, but indicated the
ensure bearing temperatures were stabilized.
temperatures was stabilizing. However, the licensee did not wait for temperature
For testing on May 1, the inspectors noted that the outboard bearing temperature  
stabilization and secured the Unit 1 TDAFW pump. The inspectors review of chart
reached 247 °F, as indicated on the chart recorders. During the PMT on May 6, some  
recorders revealed that the outboard bearing temperature was at 238 °F and still rising.
licensee personnel noted the turbine outboard bearing rising, but indicated the  
The licensee had declared the TDAFW pump operable with no PMT assessment of the
temperatures was stabilizing. However, the licensee did not wait for temperature  
outboard bearing temperature trend and no engineering analysis or evaluation of the
stabilization and secured the Unit 1 TDAFW pump. The inspectors review of chart  
changes in outboard bearing temperature from prior to the overhaul.
recorders revealed that the outboard bearing temperature was at 238 °F and still rising.
During the Unit 1 TDAFW pump quarterly IST procedure IT-8A performance on June 9,
The licensee had declared the TDAFW pump operable with no PMT assessment of the  
turbine outboard bearing temperature exceeded 225 °F. The turbine outboard bearing
outboard bearing temperature trend and no engineering analysis or evaluation of the  
temperature was at 233 °F and still rising when the pump was secured after the test was
changes in outboard bearing temperature from prior to the overhaul.  
completed. In this case, a CAP was written and a follow-up test was completed on
During the Unit 1 TDAFW pump quarterly IST procedure IT-8A performance on June 9,  
June 12, with the goal to attain bearing temperature stabilization. The test was stopped
turbine outboard bearing temperature exceeded 225 °F. The turbine outboard bearing  
at around 249.5 °F, prior to bearing temperature stabilization, and the 250 °F limit to
temperature was at 233 °F and still rising when the pump was secured after the test was  
secure the pump. The pump was declared inoperable and the plant was subsequently
completed. In this case, a CAP was written and a follow-up test was completed on  
shutdown to repair the TDAFW turbine.
June 12, with the goal to attain bearing temperature stabilization. The test was stopped  
The licensees root cause evaluation indicated the turbine was improperly assembled
at around 249.5 °F, prior to bearing temperature stabilization, and the 250 °F limit to  
during the overhaul in May 2007. In addition, the inspectors determined that changes to
secure the pump. The pump was declared inoperable and the plant was subsequently  
procedure NP 10.2.7, Post Maintenance/Return to Service Testing, did not occur when
shutdown to repair the TDAFW turbine.  
a change in the ASME OM Code in 1998 resulted in removing stabilization criteria from
The licensees root cause evaluation indicated the turbine was improperly assembled  
the normal ISTs for safety-related equipment. Specifically, the procedure allowed credit
during the overhaul in May 2007. In addition, the inspectors determined that changes to  
to be taken for ISTs; however, the procedure did not alert personnel that ISTs no longer
procedure NP 10.2.7, Post Maintenance/Return to Service Testing, did not occur when  
required temperature stabilization. Procedure NP 10.2.7, did specify that licensee
a change in the ASME OM Code in 1998 resulted in removing stabilization criteria from  
personnel review the PMT matrix for maintenance tasks performed, and the PMT matrix
the normal ISTs for safety-related equipment. Specifically, the procedure allowed credit  
specified temperature stabilization for bearing replacements. In addition, the licensee
to be taken for ISTs; however, the procedure did not alert personnel that ISTs no longer  
concluded from the root cause that: people interviewed, who were involved with the
required temperature stabilization. Procedure NP 10.2.7, did specify that licensee  
PMT recommendation, approval, and review process rely on the applicable procedure to
personnel review the PMT matrix for maintenance tasks performed, and the PMT matrix  
be correct and do not verify that the correct PMT is specified in the procedures; many
specified temperature stabilization for bearing replacements. In addition, the licensee  
operations, engineering, and planning personnel rely on memory when assigning PMT to
concluded from the root cause that: people interviewed, who were involved with the  
work that does not have a procedure-based PMT; and additional training may be
PMT recommendation, approval, and review process rely on the applicable procedure to  
necessary for PMT activities.
be correct and do not verify that the correct PMT is specified in the procedures; many  
Past Operability and Availability Analysis
operations, engineering, and planning personnel rely on memory when assigning PMT to  
From July through December 2007, the licensee evaluated the past operability and
work that does not have a procedure-based PMT; and additional training may be  
availability of the Unit 1 TDAFW pump. The inspectors, in conjunction with a technical
necessary for PMT activities.    
matter expert from the Office of Nuclear Reactor Regulation and a Regional Senior
Past Operability and Availability Analysis  
Reactor Analyst, reviewed the licensees past availability analysis, and verified the
From July through December 2007, the licensee evaluated the past operability and  
assumptions, calculations, and conclusions made by the licensee in AR 01090456, Past
availability of the Unit 1 TDAFW pump. The inspectors, in conjunction with a technical  
Availability 1P-29 Turbine Driven Auxiliary Feedwater Pump. The inspectors verified
matter expert from the Office of Nuclear Reactor Regulation and a Regional Senior  
the conclusion made by the licensee that the as-found condition of the turbine would
Reactor Analyst, reviewed the licensees past availability analysis, and verified the  
have resulted in the turbine being able to perform its function for the 24-hour mission
assumptions, calculations, and conclusions made by the licensee in AR 01090456, Past  
time. The as-found condition consisted of the following known deficiencies caused by
Availability 1P-29 Turbine Driven Auxiliary Feedwater Pump. The inspectors verified  
the spring 2007 maintenance: inadequate wheel lap setting, inadequate pump-to-turbine
the conclusion made by the licensee that the as-found condition of the turbine would  
coupling stretch; inadequate stretch and misalignment in the gear box coupling; and
have resulted in the turbine being able to perform its function for the 24-hour mission  
                                        38                                      Enclosure
time. The as-found condition consisted of the following known deficiencies caused by  
the spring 2007 maintenance: inadequate wheel lap setting, inadequate pump-to-turbine  
coupling stretch; inadequate stretch and misalignment in the gear box coupling; and  


inadequate thrust bearing axial end clearance. The basis for concluding that the
TDAFW pump would have performed its function were as follows: the accumulated run
39
time without component degradation provided indications of satisfactory operation of
Enclosure
components other than the bearing; the vibration measurements of the turbine and pump
inadequate thrust bearing axial end clearance. The basis for concluding that the  
were satisfactory and indicated normal operation; oil analysis for the bearings were
TDAFW pump would have performed its function were as follows: the accumulated run  
acceptable; IST data for the pump indicated no appreciable difference between the
time without component degradation provided indications of satisfactory operation of  
results prior to and after the overhaul of the turbine; outboard bearing temperatures,
components other than the bearing; the vibration measurements of the turbine and pump  
while significantly higher than normal, were determined via analysis by a vendor and
were satisfactory and indicated normal operation; oil analysis for the bearings were  
concurrence by the turbine manufacturer to stabilize at a temperature that was
acceptable; IST data for the pump indicated no appreciable difference between the  
acceptable for a 24-hour mission time; analysis demonstrated that adjacent turbine
results prior to and after the overhaul of the turbine; outboard bearing temperatures,  
components would not be affected by the increased bearing temperature; analysis of the
while significantly higher than normal, were determined via analysis by a vendor and  
oil at increased temperatures by the oil vendor demonstrated no significant decrease in
concurrence by the turbine manufacturer to stabilize at a temperature that was  
oil properties; and the increased bearing temperatures were evaluated by the bearing
acceptable for a 24-hour mission time; analysis demonstrated that adjacent turbine  
manufacturer and determined not to affect the operation of the bearing for a 24-hour
components would not be affected by the increased bearing temperature; analysis of the  
mission time.
oil at increased temperatures by the oil vendor demonstrated no significant decrease in  
Analysis: The inspectors determined the failure to have adequate PMT of the TDAFW
oil properties; and the increased bearing temperatures were evaluated by the bearing
pumps was a performance deficiency and a finding. Using IMC 0612, Power Reactor
manufacturer and determined not to affect the operation of the bearing for a 24-hour  
Inspection Reports, Appendix B, Issue Screening, dated September 20, 2007, the
mission time.      
inspectors determined that this finding is more than minor because if left uncorrected,
Analysis: The inspectors determined the failure to have adequate PMT of the TDAFW  
the failure would become a more significant issue.
pumps was a performance deficiency and a finding. Using IMC 0612, Power Reactor  
Using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection
Inspection Reports, Appendix B, Issue Screening, dated September 20, 2007, the  
Findings for At-Power Situations, Attachment 1, SDP Phase 1 Screening Worksheet for
inspectors determined that this finding is more than minor because if left uncorrected,  
IE, MS, and B Cornerstones, dated January 10, 2008, the inspectors determined that
the failure would become a more significant issue.
the finding did not result in an actual loss of safety function of a system or train of
Using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection  
equipment. Therefore, the finding is considered to be of very low safety significance
Findings for At-Power Situations, Attachment 1, SDP Phase 1 Screening Worksheet for  
(Green). The inspectors also determined that this finding had a cross-cutting aspect in
IE, MS, and B Cornerstones, dated January 10, 2008, the inspectors determined that  
the area of human performance because the licensee did not ensure that procedures
the finding did not result in an actual loss of safety function of a system or train of  
were adequate and accurate to assure nuclear safety (H.2(c)).
equipment. Therefore, the finding is considered to be of very low safety significance  
Enforcement: 10 CFR 50, Appendix B, Criterion V, requires, in part, that activities
(Green). The inspectors also determined that this finding had a cross-cutting aspect in  
affecting quality be prescribed and accomplished by procedures appropriate to the
the area of human performance because the licensee did not ensure that procedures  
circumstances. Contrary to this, the licensee failed to prescribe and accomplish
were adequate and accurate to assure nuclear safety (H.2(c)).  
adequate PMT with procedures appropriate to the circumstances to ensure that
Enforcement: 10 CFR 50, Appendix B, Criterion V, requires, in part, that activities  
after maintenance on safety-related equipment, the equipment returned to service
affecting quality be prescribed and accomplished by procedures appropriate to the  
in an operable condition, an activity affecting quality. Because this finding was of
circumstances. Contrary to this, the licensee failed to prescribe and accomplish  
very low safety significance (Green) and because the finding was entered into the
adequate PMT with procedures appropriate to the circumstances to ensure that  
licensees corrective action program (as CAP 01090456), this violation is being treated
after maintenance on safety-related equipment, the equipment returned to service  
as a Non-Cited Violation (NCV 05000266/2007005-05; NCV 05000301/2007005-05),
in an operable condition, an activity affecting quality. Because this finding was of  
consistent with Section VI.A of the NRC Enforcement Policy.
very low safety significance (Green) and because the finding was entered into the  
The licensee took immediate corrective actions to address the issue by revising the
licensees corrective action program (as CAP 01090456), this violation is being treated  
appropriate procedures, and at the end of the inspection period the licensee continued to
as a Non-Cited Violation (NCV 05000266/2007005-05; NCV 05000301/2007005-05),  
implement planned corrective actions.
consistent with Section VI.A of the NRC Enforcement Policy.  
                                          39                                      Enclosure
The licensee took immediate corrective actions to address the issue by revising the  
appropriate procedures, and at the end of the inspection period the licensee continued to  
implement planned corrective actions.  


.2   Evaluation of Licensees Organizational Response to the 2P-29 TDAFW Pump
    Emergent Issue (95003)
40
  b. Inspection Scope
Enclosure
    The inspectors utilized additional inspection hours allowed by IMC 0305 Operating
.2  
    Reactor Assessment Program, since Point Beach exited Column IV of the NRCs Action
Evaluation of Licensees Organizational Response to the 2P-29 TDAFW Pump  
    Matrix in 2007, to assess the licensees organizational response to a significant issue
Emergent Issue (95003)  
    associated with the Unit 2 2P-29 TDAFW pump in November 2007. In particular, the
b.  
    inspectors focused on the organizational use of human performance tools, the
Inspection Scope  
    performance of operations and engineering personnel during the issue, and utilization of
The inspectors utilized additional inspection hours allowed by IMC 0305 Operating  
    the corrective action program by the organization.
Reactor Assessment Program, since Point Beach exited Column IV of the NRCs Action  
    Increased water in the outboard bearing of TDAFW pump 2P-29 was first observed
Matrix in 2007, to assess the licensees organizational response to a significant issue  
    in June 2007. The licensee performed an operability evaluation at that time and
associated with the Unit 2 2P-29 TDAFW pump in November 2007. In particular, the  
    concluded that the pump was operable because the concentration of the oil was
inspectors focused on the organizational use of human performance tools, the  
    below the 5,000 pm threshold value for operability established by the licensee, based
performance of operations and engineering personnel during the issue, and utilization of  
    on Electric Power Research Institute (EPRI) and vendor guidance. Test results revealed
the corrective action program by the organization.  
    in June 2007 that the water concentration was approximately 140 ppm and in July
Increased water in the outboard bearing of TDAFW pump 2P-29 was first observed  
    compensatory testing identified an increase to 760 ppm. The licensee continued to
in June 2007. The licensee performed an operability evaluation at that time and  
    trend increasing water in the oil and developed a contingency plan. On September 21,
concluded that the pump was operable because the concentration of the oil was  
    the oil sample results revealed water levels had increased to 3,845 ppm, and during the
below the 5,000 pm threshold value for operability established by the licensee, based  
    2P-29 TDAFW pump run, an outboard high temperature alarm occurred. In addition,
on Electric Power Research Institute (EPRI) and vendor guidance. Test results revealed  
    operators noted that additional leakage was observed from the turbine outboard gland
in June 2007 that the water concentration was approximately 140 ppm and in July  
    area. The licensee commenced implementation of the contingency plan, which included
compensatory testing identified an increase to 760 ppm. The licensee continued to  
    a pump overhaul.
trend increasing water in the oil and developed a contingency plan. On September 21,  
    The overhaul was completed on September 23, and included replacement of the turbine
the oil sample results revealed water levels had increased to 3,845 ppm, and during the  
    shaft carbon seal rings and the turbine outboard gland seal casing. The gland and
2P-29 TDAFW pump run, an outboard high temperature alarm occurred. In addition,  
    turbine casings were then sealed with high temperature silicone per the maintenance
operators noted that additional leakage was observed from the turbine outboard gland  
    procedure. The TDAFW pump was run and oil samples were collected. The water
area. The licensee commenced implementation of the contingency plan, which included  
    content was visually estimated at 1,500 ppm, and the licensee concluded that they were
a pump overhaul.  
    within the bounds of the previous operability evaluation. A second test run conducted
The overhaul was completed on September 23, and included replacement of the turbine  
    that day revealed less water visually than the first run. Both samples were sent offsite
shaft carbon seal rings and the turbine outboard gland seal casing. The gland and  
    for analysis. On September 27, the lab results were received, with the first run showing
turbine casings were then sealed with high temperature silicone per the maintenance  
    20,400 ppm of water and the second run showing only 56 ppm of water. Condition
procedure. The TDAFW pump was run and oil samples were collected. The water  
    report CAP 01113318 was written; however, the description discounted the higher
content was visually estimated at 1,500 ppm, and the licensee concluded that they were  
    sample based on conformational biases of the personnel involved, specifically: high
within the bounds of the previous operability evaluation. A second test run conducted  
    room humidity; statements from a vendor representative noting that increased leakage
that day revealed less water visually than the first run. Both samples were sent offsite  
    may be expected following overhauls (even though this had never been seen on the
for analysis. On September 27, the lab results were received, with the first run showing  
    identical turbine for the opposite unit); and high humidity in the room where the samples
20,400 ppm of water and the second run showing only 56 ppm of water. Condition  
    were split for offsite analysis. Consequently, CAP 01113318 was closed with no action
report CAP 01113318 was written; however, the description discounted the higher  
    taken.
sample based on conformational biases of the personnel involved, specifically: high  
    On November 1, 2P-29 was run twice and the water content in the oil was analyzed
room humidity; statements from a vendor representative noting that increased leakage  
    at 29,515 ppm for the first run and 17,700 ppm for the second run, supporting the
may be expected following overhauls (even though this had never been seen on the  
    September 2007 value of 20,400 ppm of water as a valid result. The licensee
identical turbine for the opposite unit); and high humidity in the room where the samples  
    subsequently initiated its event response procedure. Revision 2 of operability
were split for offsite analysis. Consequently, CAP 01113318 was closed with no action  
    Evaluation OPR01098358 was performed and completed on November 3, and required
taken.  
    a compensatory measure of running the turbine and sampling the oil every 72 hours.
On November 1, 2P-29 was run twice and the water content in the oil was analyzed  
    Over the next several days, the TDAFW pump was run for eight hours, every 72 hours.
at 29,515 ppm for the first run and 17,700 ppm for the second run, supporting the  
                                                40                                    Enclosure
September 2007 value of 20,400 ppm of water as a valid result. The licensee  
subsequently initiated its event response procedure. Revision 2 of operability  
Evaluation OPR01098358 was performed and completed on November 3, and required  
a compensatory measure of running the turbine and sampling the oil every 72 hours.
Over the next several days, the TDAFW pump was run for eight hours, every 72 hours.


      Additional data and responses by the licensee to the inspectors questions necessitated
      three additional revisions of the OPR by November 10. On November 13, due to the
41
      continued high water content, the licensee elected to overhaul the turbine. The licensee,
Enclosure
      with vendor assistance, identified the following significant as-found conditions during the
Additional data and responses by the licensee to the inspectors questions necessitated  
      overhaul: a gap in the aluminum oil deflector ring attached to the turbine shaft by a set
three additional revisions of the OPR by November 10. On November 13, due to the  
      screw, that provided a direct path for steam to enter the bearing housing along the
continued high water content, the licensee elected to overhaul the turbine. The licensee,  
      turbine shaft; the silicone sealant, particularly around the gland housing and casing,
with vendor assistance, identified the following significant as-found conditions during the  
      exhibited a lack of adhesion, also providing a path for steam entering; and the gland
overhaul: a gap in the aluminum oil deflector ring attached to the turbine shaft by a set  
      housing, which was replaced in the September 2007 maintenance, was undersized.
screw, that provided a direct path for steam to enter the bearing housing along the  
      Following the November 2007 overhaul, the pump underwent PMT and the outboard
turbine shaft; the silicone sealant, particularly around the gland housing and casing,  
      bearing oil samples showed less than 100 ppm of water.
exhibited a lack of adhesion, also providing a path for steam entering; and the gland  
  c. Findings
housing, which was replaced in the September 2007 maintenance, was undersized.
      The inspectors identified three Green findings with associated NCVs as a result of the
Following the November 2007 overhaul, the pump underwent PMT and the outboard  
      inspection activities. Two findings are documented in this Section and a third is
bearing oil samples showed less than 100 ppm of water.  
      documented in Section 1R15.2 of this report.
c.  
b.1   Failure to Take Adequate Corrective Actions to Address Water Ingress Following
Findings  
      Maintenance
The inspectors identified three Green findings with associated NCVs as a result of the  
      Introduction: The inspectors identified a Non-Cited Violation (NCV) of 10 CFR 50,
inspection activities. Two findings are documented in this Section and a third is  
      Appendix B, Criterion XVI, Corrective Action, having very low safety significance
documented in Section 1R15.2 of this report.  
      (Green) for the licensees failure to take prompt corrective actions to correct the cause of
b.1  
      increased water in the 2P-29 TDAFW pump turbine outboard bearing housing, a
Failure to Take Adequate Corrective Actions to Address Water Ingress Following  
      condition adverse to quality, originally identified in September 2007.
Maintenance  
      Description: On September 24, 2007, following the overhaul of the 2P-29 TDAFW
Introduction: The inspectors identified a Non-Cited Violation (NCV) of 10 CFR 50,  
      pump turbine, an oil sample was taken from the outboard bearing housing, following a
Appendix B, Criterion XVI, Corrective Action, having very low safety significance  
      four hour run. CAP 01112660 was written, which documented water volume in the oil
(Green) for the licensees failure to take prompt corrective actions to correct the cause of  
      sample of 1,000 to 1,500 ppm for the four-hour run. The CAP description concluded that
increased water in the 2P-29 TDAFW pump turbine outboard bearing housing, a  
      this was an expected condition. A second shorter pump run was performed, and the
condition adverse to quality, originally identified in September 2007.  
      water content in the oil was visually estimated to be 100 ppm. The licensee rationalized
Description: On September 24, 2007, following the overhaul of the 2P-29 TDAFW  
      that the initial water content was expected and the CAP was closed with no further
pump turbine, an oil sample was taken from the outboard bearing housing, following a  
      actions taken. Three days later, CAP 01113318 was written and documented that the
four hour run. CAP 01112660 was written, which documented water volume in the oil  
      outboard oil sample from the first four-hour run was actually 20,040 ppm water, and that
sample of 1,000 to 1,500 ppm for the four-hour run. The CAP description concluded that  
      the number was not consistent with the visual indications seen on September 24. The
this was an expected condition. A second shorter pump run was performed, and the  
      description in the CAP was presented in a manner which refuted the results based on
water content in the oil was visually estimated to be 100 ppm. The licensee rationalized  
      conjecture, concluding that the 20,040 ppm results were false readings due to a
that the initial water content was expected and the CAP was closed with no further  
      laboratory error or an accidental capture of water droplets during the sampling process.
actions taken. Three days later, CAP 01113318 was written and documented that the  
      The CAP concluded that, the indicated levels of water in the IT-09A sample are errant.
outboard oil sample from the first four-hour run was actually 20,040 ppm water, and that  
      The CAP was screened by licensee staff and no additional actions were taken to either
the number was not consistent with the visual indications seen on September 24. The  
      characterize the cause of the unexplained increase of water in the oil, or to further
description in the CAP was presented in a manner which refuted the results based on  
      evaluate this unexpected condition identified through testing of the safety-related oil,
conjecture, concluding that the 20,040 ppm results were false readings due to a  
      following the four-hour TDAFW pump run. The licensee did not consider as a corrective
laboratory error or an accidental capture of water droplets during the sampling process.
      action, running the pump and obtaining another oil sample to verify that the abnormally
The CAP concluded that, the indicated levels of water in the IT-09A sample are errant.
      high water content following the overhaul was a false indication.
The CAP was screened by licensee staff and no additional actions were taken to either  
      On November 1, approximately five weeks after the maintenance overhaul, the licensee
characterize the cause of the unexplained increase of water in the oil, or to further  
      ran 2P-29 and sampled the oil. The frequency of running the pump once per month was
evaluate this unexpected condition identified through testing of the safety-related oil,  
      established in June 2007, when the moisture in the turbine outboard bearing oil was
following the four-hour TDAFW pump run. The licensee did not consider as a corrective  
                                                41                                      Enclosure
action, running the pump and obtaining another oil sample to verify that the abnormally  
high water content following the overhaul was a false indication.
On November 1, approximately five weeks after the maintenance overhaul, the licensee  
ran 2P-29 and sampled the oil. The frequency of running the pump once per month was  
established in June 2007, when the moisture in the turbine outboard bearing oil was  


significantly less than the EPRI and vendor recommended 5,000 ppm. The pump was
run slightly more than two hours and the outboard oil sample drawn revealed 29,515
42
ppm of water in the oil. After the pump had not run for about eight hours and was then
Enclosure
run for eight hours, 17,700 ppm was found in the outboard bearing oil. The licensee
significantly less than the EPRI and vendor recommended 5,000 ppm. The pump was  
declared the pump inoperable and revised the original June 2007 operability evaluation.
run slightly more than two hours and the outboard oil sample drawn revealed 29,515  
As described previously, on November 13, the licensee began an overhaul of the
ppm of water in the oil. After the pump had not run for about eight hours and was then  
turbine.
run for eight hours, 17,700 ppm was found in the outboard bearing oil. The licensee  
The inspectors determined that the original unsatisfactory oil sample results in
declared the pump inoperable and revised the original June 2007 operability evaluation.
September 2007 identified a condition adverse to quality associated with the
As described previously, on November 13, the licensee began an overhaul of the  
safety-related 2P-29 TDAFW pump; however, prompt corrective actions were not taken.
turbine.  
Analysis: The inspectors determined that the licensees failure to implement prompt
The inspectors determined that the original unsatisfactory oil sample results in  
corrective actions to address the September 2007 2P-29 TDAFW pump turbine
September 2007 identified a condition adverse to quality associated with the  
degraded oil sample results, a condition adverse to quality, was a performance
safety-related 2P-29 TDAFW pump; however, prompt corrective actions were not taken.  
deficiency and a finding. The inspectors concluded that the finding is more than minor in
Analysis: The inspectors determined that the licensees failure to implement prompt  
accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue
corrective actions to address the September 2007 2P-29 TDAFW pump turbine  
Screening, dated September 20, 2007, in that the finding could reasonably be viewed
degraded oil sample results, a condition adverse to quality, was a performance  
as a precursor to a significant event. Specifically, the failure to promptly correct the
deficiency and a finding. The inspectors concluded that the finding is more than minor in  
cause of the oil degradation in a timely manner could result in failure of the TDAFW
accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue  
turbine.
Screening, dated September 20, 2007, in that the finding could reasonably be viewed  
The significance of this finding was evaluated using IMC 0609, Appendix A,
as a precursor to a significant event. Specifically, the failure to promptly correct the  
Determining the Significance of Reactor Inspection Findings for At-Power
cause of the oil degradation in a timely manner could result in failure of the TDAFW  
Situations, dated January 10, 2008, for the Mitigating Systems Cornerstone. The
turbine.  
risk assessment for the potential loss of safety function is attributed to the performance
The significance of this finding was evaluated using IMC 0609, Appendix A,  
deficiencies associated with inadequate maintenance discussed in Section 4OA5.2.b.2
Determining the Significance of Reactor Inspection Findings for At-Power  
as URI 5000266/2007005-07. This finding, for the failure to implement prompt corrective
Situations, dated January 10, 2008, for the Mitigating Systems Cornerstone. The  
actions, did not cause the loss of safety function for greater than the allowed outage
risk assessment for the potential loss of safety function is attributed to the performance  
time. The inspectors determined that the finding is of very low safety significance
deficiencies associated with inadequate maintenance discussed in Section 4OA5.2.b.2  
(Green), because the finding did not involve a design deficiency, there was no actual
as URI 5000266/2007005-07. This finding, for the failure to implement prompt corrective  
loss of safety function, no single train loss of safety function for greater than the TS
actions, did not cause the loss of safety function for greater than the allowed outage  
allowed outage time, and no risk due to external events. The licensee concluded that
time. The inspectors determined that the finding is of very low safety significance  
although the pump was initially declared inoperable and the oil was degraded, the
(Green), because the finding did not involve a design deficiency, there was no actual  
TDAFW pump would have performed its specified safety function. Additionally, the
loss of safety function, no single train loss of safety function for greater than the TS  
inspectors determined that the finding had a cross-cutting area aspect in the area of
allowed outage time, and no risk due to external events. The licensee concluded that  
problem identification and resolution. Specifically, the licensee failed to thoroughly
although the pump was initially declared inoperable and the oil was degraded, the  
evaluate the problem with water ingress into the oil, such that a resolution addressed the
TDAFW pump would have performed its specified safety function. Additionally, the  
cause and extent of condition (P.1(c)).
inspectors determined that the finding had a cross-cutting area aspect in the area of  
Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in
problem identification and resolution. Specifically, the licensee failed to thoroughly  
part, that measures be established to assure that conditions adverse to quality, such as
evaluate the problem with water ingress into the oil, such that a resolution addressed the  
malfunctions, deficiencies, deviations, defective equipment and nonconformances are
cause and extent of condition (P.1(c)).  
promptly identified and corrected. Contrary to this, a condition adverse to quality,
Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in  
associated with the turbine of the Unit 2 TDAFW pump 2P-29 was not promptly
part, that measures be established to assure that conditions adverse to quality, such as  
corrected following identification in September 2007. Specifically, upon identification of
malfunctions, deficiencies, deviations, defective equipment and nonconformances are  
degraded oil in September 2007, a condition adverse to quality, the licensee did not take
promptly identified and corrected. Contrary to this, a condition adverse to quality,  
prompt corrective actions. As a result of the failure to take prompt corrective actions, the
associated with the turbine of the Unit 2 TDAFW pump 2P-29 was not promptly  
pump was declared inoperable until November 2007, following additional oil samples
corrected following identification in September 2007. Specifically, upon identification of  
that revealed the continued degraded condition. Because of the very low safety
degraded oil in September 2007, a condition adverse to quality, the licensee did not take  
significance of this finding and because it was entered into the licensees corrective
prompt corrective actions. As a result of the failure to take prompt corrective actions, the  
                                          42                                        Enclosure
pump was declared inoperable until November 2007, following additional oil samples  
that revealed the continued degraded condition. Because of the very low safety  
significance of this finding and because it was entered into the licensees corrective  


    action program as CAP 01115748, this violation is being treated as an NCV, consistent
    with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000301/2007005-06).
43
    The licensee took immediate corrective actions to address the issue, which included
Enclosure
    reevaluation of operability and ultimately overhaul of 2P-29, and at the end of the
action program as CAP 01115748, this violation is being treated as an NCV, consistent  
    inspection period the licensee continued to evaluate the causes associated with this
with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000301/2007005-06).  
    finding.
The licensee took immediate corrective actions to address the issue, which included  
b.2 Unresolved Item: Failure to Perform Adequate Maintenance Resulting in Increased
reevaluation of operability and ultimately overhaul of 2P-29, and at the end of the  
    Water Ingress
inspection period the licensee continued to evaluate the causes associated with this  
    Introduction: The inspectors identified a URI associated with the licensees failure to
finding.  
    perform adequate maintenance on the Unit 2 TDAFW pump turbine in September 2007.
b.2  
    Description: The elevated moisture content in the outboard bearing for the 2P-29 turbine
Unresolved Item: Failure to Perform Adequate Maintenance Resulting in Increased  
    was present since the last ten-year overhaul was performed in November 2006.
Water Ingress  
    However, while the moisture content levels in the oil from November 2006 until the
Introduction: The inspectors identified a URI associated with the licensees failure to  
    September 21, 2007, overhaul were elevated, the levels were below the 5,000 ppm
perform adequate maintenance on the Unit 2 TDAFW pump turbine in September 2007.  
    value documented as acceptable in EPRI and vendor guidance. Steam leakage from
Description: The elevated moisture content in the outboard bearing for the 2P-29 turbine  
    the gland seal or turbine casing joints prior to the September overhaul would not have
was present since the last ten-year overhaul was performed in November 2006.
    been vented away from the bearing housing since the turbine insulation extended over
However, while the moisture content levels in the oil from November 2006 until the  
    the top of the gland seal casing and up to the bearing housing. In addition, original
September 21, 2007, overhaul were elevated, the levels were below the 5,000 ppm  
    cement-based insulation also blocked the gland seal area vent holes.
value documented as acceptable in EPRI and vendor guidance. Steam leakage from  
    The licensee concluded, based on test data, that the 2P-29 turbine overhaul that was
the gland seal or turbine casing joints prior to the September overhaul would not have  
    completed on September 23, 2007, significantly increased the moisture content in the
been vented away from the bearing housing since the turbine insulation extended over  
    outboard bearing oil. A silicone seal applied at the gland casing to turbine casing joint
the top of the gland seal casing and up to the bearing housing. In addition, original  
    failed upon initial service resulting in a steam leak in the area of the outboard bearing
cement-based insulation also blocked the gland seal area vent holes.  
    housing. The failure of the sealant could not be attributed to one factor; however, the
The licensee concluded, based on test data, that the 2P-29 turbine overhaul that was  
    licensee did conclude one of the root causes was its maintenance procedures did not
completed on September 23, 2007, significantly increased the moisture content in the  
    address the special requirements needed when applying sealants, and, therefore, site
outboard bearing oil. A silicone seal applied at the gland casing to turbine casing joint  
    personnel did not have adequate instruction or training on the use of sealants. In
failed upon initial service resulting in a steam leak in the area of the outboard bearing  
    addition, the licensee identified that the September 2007 maintenance did not allow for
housing. The failure of the sealant could not be attributed to one factor; however, the  
    the proper cure time of 24 hours for the sealant and exceeded the process time of 30
licensee did conclude one of the root causes was its maintenance procedures did not  
    minutes from when the sealant was applied and the joint was torqued.
address the special requirements needed when applying sealants, and, therefore, site  
    In a review of the site maintenance procedures, the licensee also identified an additional
personnel did not have adequate instruction or training on the use of sealants. In  
    root cause that the site continued to lack adequate guidance on specific assembly
addition, the licensee identified that the September 2007 maintenance did not allow for  
    details of the turbine, specifically for the oil deflector ring on the turbine shaft: the
the proper cure time of 24 hours for the sealant and exceeded the process time of 30  
    tightening of the oil deflector ring set screw was not discussed; and acceptable
minutes from when the sealant was applied and the joint was torqued.  
    clearances between the turbine shaft and the inner diameter of the oil deflector ring were
In a review of the site maintenance procedures, the licensee also identified an additional  
    not specified.
root cause that the site continued to lack adequate guidance on specific assembly  
    The licensee identified three additional contributing causes: receipt and installation of a
details of the turbine, specifically for the oil deflector ring on the turbine shaft: the  
    gland casing from the vendor that had incorrect critical dimensions; previous insulation
tightening of the oil deflector ring set screw was not discussed; and acceptable  
    work blocked the gland seal vents; and plant personnel did not have adequate guidance
clearances between the turbine shaft and the inner diameter of the oil deflector ring were  
    on the installation of insulation. At the end of the inspection period, the licensee
not specified.
    continued to develop and implement corrective actions to address the issues
The licensee identified three additional contributing causes: receipt and installation of a  
    documented in CAP 01115748.
gland casing from the vendor that had incorrect critical dimensions; previous insulation  
                                                43                                        Enclosure
work blocked the gland seal vents; and plant personnel did not have adequate guidance  
on the installation of insulation. At the end of the inspection period, the licensee  
continued to develop and implement corrective actions to address the issues  
documented in CAP 01115748.  


    At the conclusion of the inspection, the licensee continued to assess the impact of the
    water ingress on the availability of the Unit 2 TDAFW pump to perform its design and
44
    augmented quality functions. There is no current safety concern because the pump was
Enclosure
    adequately tested and the current low ingress of water into the bearing housing indicated
At the conclusion of the inspection, the licensee continued to assess the impact of the  
    that the pumps functionality is currently maintained for all licensing and design basis
water ingress on the availability of the Unit 2 TDAFW pump to perform its design and  
    events. This issue is an Unresolved Item (URI 05000301/2007005-07) until the NRC
augmented quality functions. There is no current safety concern because the pump was  
    reviews the licensees past availability assessment.
adequately tested and the current low ingress of water into the bearing housing indicated  
.3   Evaluation of the Licensees Independent Assessment of Engineering (95003)
that the pumps functionality is currently maintained for all licensing and design basis  
  a. Inspection Scope
events. This issue is an Unresolved Item (URI 05000301/2007005-07) until the NRC  
    The inspectors utilized additional inspection hours allowed by IMC 0305, since Point
reviews the licensees past availability assessment.  
    Beach exited Column IV of the NRCs Action Matrix in 2007, to assess the licensees
.3  
    independent assessment of engineering. The licensee committed as part of its response
Evaluation of the Licensees Independent Assessment of Engineering (95003)  
    to the Confirmatory Action Letter CAL 3-04-001, Revision 1, dated April 14, 2006, to
a.  
    perform alternating independent and self-assessments of the engineering and corrective
Inspection Scope  
    action programs. In July 2007, the licensee performed an independent assessment of
The inspectors utilized additional inspection hours allowed by IMC 0305, since Point  
    engineering performance. The inspectors reviewed the charter for the assessment,
Beach exited Column IV of the NRCs Action Matrix in 2007, to assess the licensees  
    observed the independent assessment team, reviewed the final report, and reviewed the
independent assessment of engineering. The licensee committed as part of its response  
    proposed corrective actions.
to the Confirmatory Action Letter CAL 3-04-001, Revision 1, dated April 14, 2006, to  
  b. Observations and Assessment
perform alternating independent and self-assessments of the engineering and corrective  
    The team consisted of four experienced individuals from other utilities and a consulting
action programs. In July 2007, the licensee performed an independent assessment of  
    firm. The team assessed licensee engineering performance in five areas: fundamentals
engineering performance. The inspectors reviewed the charter for the assessment,  
    of engineering, equipment reliability, configuration management, corrective actions, and
observed the independent assessment team, reviewed the final report, and reviewed the  
    operating experience. The assessment teams overall conclusions were: engineering
proposed corrective actions.    
    rigor and overall quality has improved and has been sufficient for successful
b.  
    management of potential challenges to design bases and equipment reliability;
Observations and Assessment  
    unresolved plant material conditions present substantial ongoing challenges; a plateau
The team consisted of four experienced individuals from other utilities and a consulting  
    may have been reached for engineering improvement; and additional resources and
firm. The team assessed licensee engineering performance in five areas: fundamentals  
    continued effort will be required to sustain the improvements that have already been
of engineering, equipment reliability, configuration management, corrective actions, and  
    obtained and to bridge the remaining gaps to engineering excellence.
operating experience. The assessment teams overall conclusions were: engineering  
    The assessment team identified the following overall issues for attention: most recent
rigor and overall quality has improved and has been sufficient for successful  
    engineering products are of high quality, but examples of products with less than
management of potential challenges to design bases and equipment reliability;  
    adequate rigor are still produced; engineering needs to be more predictable and
unresolved plant material conditions present substantial ongoing challenges; a plateau  
    accountable with respect to schedules; important longstanding issues were not resolved;
may have been reached for engineering improvement; and additional resources and  
    engineering resources may not be adequately matched to engineering obligations; the
continued effort will be required to sustain the improvements that have already been  
    preventive maintenance optimization and single point vulnerability projects have
obtained and to bridge the remaining gaps to engineering excellence.  
    languished and, as a consequence, the station had not benefited from the improved
The assessment team identified the following overall issues for attention: most recent  
    material condition and safety margins; although a list of low margin issues had been
engineering products are of high quality, but examples of products with less than  
    established, there did not appear to be a quantification of the lost margin associated with
adequate rigor are still produced; engineering needs to be more predictable and  
    these issues or an evaluation of the cumulative effects; it was not clear that cumulative
accountable with respect to schedules; important longstanding issues were not resolved;  
    effects of conditions adverse to quality were being addressed and the large number of
engineering resources may not be adequately matched to engineering obligations; the  
    open conditions presented a challenge to effectiveness of such a review; and the
preventive maintenance optimization and single point vulnerability projects have  
    corrective action process was not used to the full potential, specifically: trending was not
languished and, as a consequence, the station had not benefited from the improved  
    being used as effectively as it could be; more effective use of corrective action
material condition and safety margins; although a list of low margin issues had been  
    processes for vendor products was warranted; and expectations for a close to fix
established, there did not appear to be a quantification of the lost margin associated with  
    solution, versus an apparent cause evaluation warranted examination.
these issues or an evaluation of the cumulative effects; it was not clear that cumulative  
                                              44                                      Enclosure
effects of conditions adverse to quality were being addressed and the large number of  
open conditions presented a challenge to effectiveness of such a review; and the  
corrective action process was not used to the full potential, specifically: trending was not  
being used as effectively as it could be; more effective use of corrective action  
processes for vendor products was warranted; and expectations for a close to fix  
solution, versus an apparent cause evaluation warranted examination.  


    The overall recommendations from the assessment team were 1) to maintain highly
    visible management commitment to rigor and continue associated empowerment, and
45
    2) to implement the specifically identified corrective actions for issues with predictability,
Enclosure
    resolution of longstanding issues, prevent maintenance optimization, cumulative effects
The overall recommendations from the assessment team were 1) to maintain highly  
    of material condition, more aggressive use of corrective action processes, margin
visible management commitment to rigor and continue associated empowerment, and  
    issues, and engineering resources.
2) to implement the specifically identified corrective actions for issues with predictability,  
    The inspectors confirmed that the licensee had developed plans and corrective actions
resolution of longstanding issues, prevent maintenance optimization, cumulative effects  
    to address the issues for attention identified by the Independent Assessment Team.
of material condition, more aggressive use of corrective action processes, margin  
.4   Evaluation of the Independent Assessment of the Corrective Action Program (95003)
issues, and engineering resources.  
  a. Inspection Scope
The inspectors confirmed that the licensee had developed plans and corrective actions  
    The inspectors utilized additional inspection hours allowed by IMC 0305, since Point
to address the issues for attention identified by the Independent Assessment Team.  
    Beach exited Column IV of the NRCs Action Matrix in 2007, to assess the licensees
.4  
    independent assessment of the corrective action program. The licensee committed as
Evaluation of the Independent Assessment of the Corrective Action Program (95003)  
    part of its response to the Confirmatory Action Letter CAL 3-04-001, Revision 1, dated
a.  
    April 14, 2006, to perform alternating independent and self-assessments of the
Inspection Scope  
    engineering and corrective action programs. The inspectors reviewed the charter for the
The inspectors utilized additional inspection hours allowed by IMC 0305, since Point  
    assessment of the corrective action program in August 2007, observed the independent
Beach exited Column IV of the NRCs Action Matrix in 2007, to assess the licensees  
    assessment team, reviewed the final report, and reviewed the proposed corrective
independent assessment of the corrective action program. The licensee committed as  
    actions.
part of its response to the Confirmatory Action Letter CAL 3-04-001, Revision 1, dated  
  b. Observations and Assessment
April 14, 2006, to perform alternating independent and self-assessments of the  
    The team consisted of four experienced individuals from other utilities and a consulting
engineering and corrective action programs. The inspectors reviewed the charter for the  
    firm. The team concluded that although measurable improvement in the corrective
assessment of the corrective action program in August 2007, observed the independent  
    action program had been achieved over the last 12 months, several opportunities for
assessment team, reviewed the final report, and reviewed the proposed corrective  
    improvement needed to be addressed in order to achieve improved performance. The
actions.  
    team noted the following opportunities for improvement: the effectiveness and quality of
b.  
    apparent cause evaluations needed to be improved; the number of corrective action
Observations and Assessment  
    program performance indicators above target with no detailed recovery plan indicated
The team consisted of four experienced individuals from other utilities and a consulting  
    that timeliness continued to be an issue, corrective action program backlog, in particular,
firm. The team concluded that although measurable improvement in the corrective  
    has been increasing; the ease of CAP initiation via computer (Passport software) and
action program had been achieved over the last 12 months, several opportunities for  
    providing feedback to the CAP initiator for CAPs which are closed by the management
improvement needed to be addressed in order to achieve improved performance. The  
    screening committee with no action; trending has not been effective at identifying
team noted the following opportunities for improvement: the effectiveness and quality of  
    adverse trends through the quarterly Department Roll-Up Meetings and Passport issues
apparent cause evaluations needed to be improved; the number of corrective action  
    continue to impede trending; effectiveness reviews for corrective actions to prevent
program performance indicators above target with no detailed recovery plan indicated  
    recurrence needed to consider effectiveness from a broader perspective; additional
that timeliness continued to be an issue, corrective action program backlog, in particular,  
    opportunities for improvement were identified in apparent cause evaluations for NRC-
has been increasing; the ease of CAP initiation via computer (Passport software) and  
    identified findings and on the effectiveness of certain actions specified to correct the
providing feedback to the CAP initiator for CAPs which are closed by the management  
    January 2007 corrective action program self-assessment issues.
screening committee with no action; trending has not been effective at identifying  
    The independent assessment team concluded that some positive features of the
adverse trends through the quarterly Department Roll-Up Meetings and Passport issues  
    corrective action program included: management was highly engaged in the program
continue to impede trending; effectiveness reviews for corrective actions to prevent  
    and the screening committee appears to be highly effective; root cause evaluations were
recurrence needed to consider effectiveness from a broader perspective; additional  
    thorough and comprehensive, and effectiveness review criteria were clearly specified;
opportunities for improvement were identified in apparent cause evaluations for NRC-
    format consistency has improved for apparent cause evaluations, effectiveness reviews,
identified findings and on the effectiveness of certain actions specified to correct the  
    and department roll-up meeting reports; the Performance Assessment Review Board
January 2007 corrective action program self-assessment issues.  
    was involved in reviewing the backlog of open CAPs by department; and most actions
The independent assessment team concluded that some positive features of the  
                                              45                                      Enclosure
corrective action program included: management was highly engaged in the program  
and the screening committee appears to be highly effective; root cause evaluations were  
thorough and comprehensive, and effectiveness review criteria were clearly specified;  
format consistency has improved for apparent cause evaluations, effectiveness reviews,  
and department roll-up meeting reports; the Performance Assessment Review Board  
was involved in reviewing the backlog of open CAPs by department; and most actions  


  taken to address issues from the January 2007 corrective action program self-
  assessment had resulted in measurable improvement.
46
  The inspectors confirmed that the licensee had developed plans and corrective actions
Enclosure
  to address the opportunities for improvement identified by the Independent Assessment
taken to address issues from the January 2007 corrective action program self-
  Team.
assessment had resulted in measurable improvement.  
.5 (Closed) URI 05000266/2006004-05; 05000301/2006004-05: Inadequate 10 CFR 72.48
The inspectors confirmed that the licensee had developed plans and corrective actions  
    Screening to Evaluate Possible Thermal Effects on Fuel Cladding
to address the opportunities for improvement identified by the Independent Assessment  
  Introduction: The inspectors identified one violation of 10 CFR 72.48(c)(1) in which the
Team.  
  licensee failed to obtain a Certificate of Compliance (CoC) amendment pursuant to
.5  
  10 CFR 72.244 for changes made in the spent fuel storage cask operating procedures
(Closed) URI 05000266/2006004-05; 05000301/2006004-05: Inadequate 10 CFR 72.48  
  during the 2004 loading campaign as described in the FSAR and these changes in the
Screening to Evaluate Possible Thermal Effects on Fuel Cladding  
  procedures constituted a change in the terms, conditions, or specifications incorporated
Introduction: The inspectors identified one violation of 10 CFR 72.48(c)(1) in which the  
  in the CoC. Specifically, although Point Beach changed an operating procedure
licensee failed to obtain a Certificate of Compliance (CoC) amendment pursuant to  
  described in the FSAR that allowed pump down of water from the dry shielded canister
10 CFR 72.244 for changes made in the spent fuel storage cask operating procedures  
  to occur much earlier in the process; Point Beach failed to identify that the following TS,
during the 2004 loading campaign as described in the FSAR and these changes in the  
  which was incorporated in the CoC, would have required changes that needed prior
procedures constituted a change in the terms, conditions, or specifications incorporated  
  NRC approval: TS 1.2.17a, 32PT Dry Storage Canister (DSC) Vacuum Drying Duration
in the CoC. Specifically, although Point Beach changed an operating procedure  
  Limit.
described in the FSAR that allowed pump down of water from the dry shielded canister  
  Description: During the fall 2004 campaign, the licensee used the new NUHOMS 32-PT
to occur much earlier in the process; Point Beach failed to identify that the following TS,  
  cask design and modified the sequence of its loading procedures from the generic
which was incorporated in the CoC, would have required changes that needed prior  
  operating procedures stated in Chapter M.8 of the FSAR. The change consisted of
NRC approval: TS 1.2.17a, 32PT Dry Storage Canister (DSC) Vacuum Drying Duration  
  draining all of the water from the canister cavity prior to welding the inner top cover on,
Limit.  
  whereas the FSAR prescribed draining some of the water from the canister
Description: During the fall 2004 campaign, the licensee used the new NUHOMS 32-PT  
  (approximately 750 gallons), then welding the top inner cover and then draining the
cask design and modified the sequence of its loading procedures from the generic  
  remainder of the water from the canister. In the 10 CFR 72.48 screening, the licensee
operating procedures stated in Chapter M.8 of the FSAR. The change consisted of  
  failed to evaluate the effect of the water removal during draining and welding on the fuel
draining all of the water from the canister cavity prior to welding the inner top cover on,  
  cladding temperature. The inadequate screening failed to identify that TS 1.2.17a,
whereas the FSAR prescribed draining some of the water from the canister  
  32 PT DSC Vacuum Drying Duration Limit, which was incorporated in the CoC, would
(approximately 750 gallons), then welding the top inner cover and then draining the  
  have required a change that needed prior NRC approval. This amendment to the CoC
remainder of the water from the canister. In the 10 CFR 72.48 screening, the licensee  
  would address any affects on the vacuum drying time limits that may result from the
failed to evaluate the effect of the water removal during draining and welding on the fuel  
  potentially higher fuel cladding temperature. The initial fuel cladding temperature, at the
cladding temperature. The inadequate screening failed to identify that TS 1.2.17a,  
  start of vacuum drying in the procedure that deviated from the FSAR, could be higher
32 PT DSC Vacuum Drying Duration Limit, which was incorporated in the CoC, would  
  than the FSAR assumed value of 215 °F. An assumed temperature of the fuel cladding
have required a change that needed prior NRC approval. This amendment to the CoC  
  higher than the 215 °F basis in the FSAR may result in a shorter vacuum drying time
would address any affects on the vacuum drying time limits that may result from the  
  than that specified in TS 1.2.17a. The licensee loaded five casks utilizing the different
potentially higher fuel cladding temperature. The initial fuel cladding temperature, at the  
  loading process.
start of vacuum drying in the procedure that deviated from the FSAR, could be higher  
  Subsequently, in 2006, the licensees cask vendor, Transnuclear, performed a NUHOMS
than the FSAR assumed value of 215 °F. An assumed temperature of the fuel cladding  
  32PT drain down evaluation (Calculation No. NU32PT-0420) to address the issues with
higher than the 215 °F basis in the FSAR may result in a shorter vacuum drying time  
  the vacuum drying duration limit and fuel cladding temperature. The inspectors
than that specified in TS 1.2.17a. The licensee loaded five casks utilizing the different  
  reviewed the calculation, which concluded that the maximum fuel cladding temperature
loading process.  
  for the 32PT DSC with a heat load of 16.88 kilowatts (kW) (highest heat load for the
Subsequently, in 2006, the licensees cask vendor, Transnuclear, performed a NUHOMS  
  32PT DSC amongst users of this canister at the time) was 720 °F. The 720 °F
32PT drain down evaluation (Calculation No. NU32PT-0420) to address the issues with  
  temperature was below the allowable limit of 752 °F. Therefore, no time limitation was
the vacuum drying duration limit and fuel cladding temperature. The inspectors  
  necessary for vacuum drying of the 32PT DSC when the total decay heat load was
reviewed the calculation, which concluded that the maximum fuel cladding temperature  
  16.88 kW or below.
for the 32PT DSC with a heat load of 16.88 kilowatts (kW) (highest heat load for the  
                                              46                                      Enclosure
32PT DSC amongst users of this canister at the time) was 720 °F. The 720 °F  
temperature was below the allowable limit of 752 °F. Therefore, no time limitation was  
necessary for vacuum drying of the 32PT DSC when the total decay heat load was  
16.88 kW or below.  


Transnuclear also performed another evaluation (Calculation NUH32PT-0421) in which it
modeled a loading configuration that resulted in the maximum fuel cladding temperature
47
for vacuum drying. This loading configuration produced a 22.4 kW total heat load.
Enclosure
TS 1.2.17a stated that the limit for duration of vacuum drying was 31 hours for a 32PT
Transnuclear also performed another evaluation (Calculation NUH32PT-0421) in which it  
DSC with a heat load greater than 8.4 kW and up to 24 kW after initiation of vacuum
modeled a loading configuration that resulted in the maximum fuel cladding temperature  
drying. This value of 22.4 kW total maximum heat load was within the maximum TS fuel
for vacuum drying. This loading configuration produced a 22.4 kW total heat load.
cladding temperature for the 24 kW heat load. The results of this evaluation justified
TS 1.2.17a stated that the limit for duration of vacuum drying was 31 hours for a 32PT  
using a constant temperature of 215 °F for DSC during handling, welding, and vacuum
DSC with a heat load greater than 8.4 kW and up to 24 kW after initiation of vacuum  
drying operations, and indicated that after 31 hours of vacuum drying the maximum fuel
drying. This value of 22.4 kW total maximum heat load was within the maximum TS fuel  
cladding temperature was 739 °F, below the allowable limit of 752 °F. The maximum
cladding temperature for the 24 kW heat load. The results of this evaluation justified  
fuel cladding temperature reached the allowable limit of 752 °F at 67 hours after the start
using a constant temperature of 215 °F for DSC during handling, welding, and vacuum  
of the DSC drainage. Thus, the evaluation concluded that the time limit of 31 hours for
drying operations, and indicated that after 31 hours of vacuum drying the maximum fuel  
vacuum drying was acceptable.
cladding temperature was 739 °F, below the allowable limit of 752 °F. The maximum  
Analysis: The inspectors determined that the failure to obtain a CoC amendment
fuel cladding temperature reached the allowable limit of 752 °F at 67 hours after the start  
pursuant to 10 CFR 72.244 for changes made in the spent fuel storage cask operating
of the DSC drainage. Thus, the evaluation concluded that the time limit of 31 hours for  
procedures, as described in the FSAR, was a performance deficiency and a finding.
vacuum drying was acceptable.  
This finding is more than minor because it had the potential to impact the NRCs ability
Analysis: The inspectors determined that the failure to obtain a CoC amendment  
to perform its regulatory function, since the licensee failed to receive NRC approval for a
pursuant to 10 CFR 72.244 for changes made in the spent fuel storage cask operating  
change in this licensed activity. A CoC amendment was required since these changes in
procedures, as described in the FSAR, was a performance deficiency and a finding.
the procedures constituted a change in the terms, conditions, or specifications
This finding is more than minor because it had the potential to impact the NRCs ability  
incorporated into the CoC. The inspectors determined that the finding was not suitable
to perform its regulatory function, since the licensee failed to receive NRC approval for a  
for SDP evaluation because the noncompliance involved 10 CFR Part 72 dry fuel
change in this licensed activity. A CoC amendment was required since these changes in  
storage activities. Therefore, this finding was reviewed by Regional Management and
the procedures constituted a change in the terms, conditions, or specifications  
dispositioned using traditional enforcement.
incorporated into the CoC. The inspectors determined that the finding was not suitable  
Enforcement: 10 CFR 72.48(c)(1) states, in part, that a certificate holder may make
for SDP evaluation because the noncompliance involved 10 CFR Part 72 dry fuel  
changes in the facility or spent fuel storage cask design as described in the FSAR (as
storage activities. Therefore, this finding was reviewed by Regional Management and  
updated), make changes in the procedures as described in the FSAR (as updated),
dispositioned using traditional enforcement.  
without obtaining: (a) a Certificate of Compliance (CoC) amendment submitted by the
Enforcement: 10 CFR 72.48(c)(1) states, in part, that a certificate holder may make  
certificate holder pursuant to 10 CFR 72.244; if: (b) a change in the terms conditions, or
changes in the facility or spent fuel storage cask design as described in the FSAR (as  
specifications incorporated in the CoC is not required; and (c) the change, test, or
updated), make changes in the procedures as described in the FSAR (as updated),  
experiment does not meet any of the criteria in paragraph in 10 CFR 72.48(c)(2).
without obtaining: (a) a Certificate of Compliance (CoC) amendment submitted by the  
Contrary to this, in an approved 10 CFR 72.48 evaluation, Point Beach failed to obtain a
certificate holder pursuant to 10 CFR 72.244; if: (b) a change in the terms conditions, or  
CoC amendment pursuant to 10 CFR 72.244 for changes made in the spent fuel storage
specifications incorporated in the CoC is not required; and (c) the change, test, or  
cask operating procedures as described in the FSAR (as updated) and these changes in
experiment does not meet any of the criteria in paragraph in 10 CFR 72.48(c)(2).  
the procedures constituted a change in the terms, conditions, or specifications
Contrary to this, in an approved 10 CFR 72.48 evaluation, Point Beach failed to obtain a  
incorporated in the CoC. Specifically, although Point Beach changed an operating
CoC amendment pursuant to 10 CFR 72.244 for changes made in the spent fuel storage  
procedure described in the FSAR which allowed pump down of water from the dry
cask operating procedures as described in the FSAR (as updated) and these changes in  
shielded canister to occur much earlier in the process; Point Beach failed to identify that
the procedures constituted a change in the terms, conditions, or specifications  
the following TS, which was incorporated in the CoC, would have required changes that
incorporated in the CoC. Specifically, although Point Beach changed an operating  
needed prior NRC approval: TS 1.2.17a, 32PT DSC Vacuum Drying Duration Limit.
procedure described in the FSAR which allowed pump down of water from the dry  
Because this violation was of very low safety significance, was not repetitive or willful,
shielded canister to occur much earlier in the process; Point Beach failed to identify that  
and was entered into your corrective action program, this violation is being treated as an
the following TS, which was incorporated in the CoC, would have required changes that  
NCV of 10 CFR 72.48(c)(1), consistent with Section VI.A.1 of the NRC Enforcement
needed prior NRC approval: TS 1.2.17a, 32PT DSC Vacuum Drying Duration Limit.
Policy (NCV 05000266/2007005-09; 05000301/2007005-09).
Because this violation was of very low safety significance, was not repetitive or willful,  
The licensee entered the issue into the corrective action program as CAP 01026070 and
and was entered into your corrective action program, this violation is being treated as an  
implemented corrective actions, including revising the loading procedure to reflect the
NCV of 10 CFR 72.48(c)(1), consistent with Section VI.A.1 of the NRC Enforcement  
sequence described in the FSAR prior to loading the next cask (cask 6).
Policy (NCV 05000266/2007005-09; 05000301/2007005-09).  
                                          47                                    Enclosure
The licensee entered the issue into the corrective action program as CAP 01026070 and  
implemented corrective actions, including revising the loading procedure to reflect the  
sequence described in the FSAR prior to loading the next cask (cask 6).  


  .6 (Closed) URI 07200005/2004003-01: Adequacy of Design Calculation,
   
      PBNP-305336-SO1
48
    During an October through December 2004 NRC inspection, inspectors identified one
Enclosure
    URI associated with the adequacy of the licensees auxiliary building structure and the
.6  
    crane design basis during a seismic event. The licensee received an NCV of
(Closed) URI 07200005/2004003-01: Adequacy of Design Calculation,  
    10 CFR 72.122(2)(i), documented in Inspection Report 07200005/2004-003(DNMS),
PBNP-305336-SO1  
    regarding failure to demonstrate that the crane, a component important to safety, was
During an October through December 2004 NRC inspection, inspectors identified one  
    designed to withstand the effects of an earthquake without impairing its capability to
URI associated with the adequacy of the licensees auxiliary building structure and the  
    perform its intended function. Upon further review, the inspectors identified other
crane design basis during a seismic event. The licensee received an NCV of  
    deficiencies in the structural analysis of the building and the crane for which the URI was
10 CFR 72.122(2)(i), documented in Inspection Report 07200005/2004-003(DNMS),  
    opened. There was no response spectra analysis performed on the building to model its
regarding failure to demonstrate that the crane, a component important to safety, was  
    response due to an earthquake at different elevations, such as that of the crane. Also,
designed to withstand the effects of an earthquake without impairing its capability to  
    the inspectors could not independently verify that the basis for the horizontal
perform its intended function. Upon further review, the inspectors identified other  
    accelerations in all of the calculations used for the auxiliary building and the crane were
deficiencies in the structural analysis of the building and the crane for which the URI was  
    adequate. In response to these questions, the licensee constructed a detailed computer
opened. There was no response spectra analysis performed on the building to model its  
    model of the steel portion of the auxiliary building. The preliminary results from an
response due to an earthquake at different elevations, such as that of the crane. Also,  
    analysis using this model demonstrated that the original acceleration values were
the inspectors could not independently verify that the basis for the horizontal  
    conservative and adequate to demonstrate compliance with regulations and the ability of
accelerations in all of the calculations used for the auxiliary building and the crane were  
    the building and the crane to sustain up to a 125-ton load under an earthquake scenario.
adequate. In response to these questions, the licensee constructed a detailed computer  
    In addition, the licensee hired an independent consultant who confirmed the licensee=s
model of the steel portion of the auxiliary building. The preliminary results from an  
    results. The inspectors were not able to validate these conclusions since the
analysis using this model demonstrated that the original acceleration values were  
    appropriate documentation was not available at the time of the inspection and a
conservative and adequate to demonstrate compliance with regulations and the ability of  
    complete analysis was not completed. However, the licensee committed to perform a
the building and the crane to sustain up to a 125-ton load under an earthquake scenario.
    full analysis of the auxiliary building and the crane response under a seismic event with
In addition, the licensee hired an independent consultant who confirmed the licensee=s  
    the current plant conditions.
results. The inspectors were not able to validate these conclusions since the  
    The licensee performed an analysis of the Class 3 Primary Auxiliary Building (PAB)
appropriate documentation was not available at the time of the inspection and a  
    Steel Superstructure in Calculation PBNP-305336-SO1, Structural Analysis of Central
complete analysis was not completed. However, the licensee committed to perform a  
    PAB with Crane Load of 125 Tons, Revision 1, dated April 3, 2006. During the current
full analysis of the auxiliary building and the crane response under a seismic event with  
    inspection, NRC staff reviewed the calculation results and discussed the assumptions
the current plant conditions.
    with licensee personnel. The analysis demonstrated the capability of the structure to
The licensee performed an analysis of the Class 3 Primary Auxiliary Building (PAB)  
    support the crane with a load of 125 tons in case of a seismic event once the welded
Steel Superstructure in Calculation PBNP-305336-SO1, Structural Analysis of Central  
    connection of the gusset and Columns 10U and 13U were strengthened. Thus, the
PAB with Crane Load of 125 Tons, Revision 1, dated April 3, 2006. During the current  
    calculation verified that the requirements of NUREG-0612 and 10 CFR 72.122(b)(2)(i)
inspection, NRC staff reviewed the calculation results and discussed the assumptions  
    were satisfied. The inspectors concluded that the revised calculation was adequate to
with licensee personnel. The analysis demonstrated the capability of the structure to  
    demonstrate compliance with regulations and the ability of the building and the crane to
support the crane with a load of 125 tons in case of a seismic event once the welded  
    sustain up to a 125-ton load under an earthquake scenario.
connection of the gusset and Columns 10U and 13U were strengthened. Thus, the  
4OA6 MANAGEMENT MEETINGS
calculation verified that the requirements of NUREG-0612 and 10 CFR 72.122(b)(2)(i)  
.1 Exit Meeting Summary
were satisfied. The inspectors concluded that the revised calculation was adequate to  
    On January 10, 2008, the inspectors presented the inspection results to Mr. James
demonstrate compliance with regulations and the ability of the building and the crane to  
    McCarthy and other members of the licensee staff. The licensee acknowledged the
sustain up to a 125-ton load under an earthquake scenario.  
    issues presented. The inspectors asked the licensee whether any materials examined
4OA6 MANAGEMENT MEETINGS  
    during the inspection should be considered proprietary. No proprietary information was
.1  
    identified.
Exit Meeting Summary  
                                                48                                      Enclosure
On January 10, 2008, the inspectors presented the inspection results to Mr. James  
McCarthy and other members of the licensee staff. The licensee acknowledged the  
issues presented. The inspectors asked the licensee whether any materials examined  
during the inspection should be considered proprietary. No proprietary information was  
identified.  


  .2 Interim Exit Meeting
   
    An interim exit meeting was conducted for:
49
    *       Maintenance Effectiveness Periodic Evaluation with Mr. Walt Smith,
Enclosure
            Acting Plant Manager on November 2, 2007.
.2  
    *       Biennial Licensed Operator Requalification Program Inspection with
Interim Exit Meeting  
            Mr. J. McCarthy on November 9, 2007.
An interim exit meeting was conducted for:  
    *       Overall assessments of the annual operating test via telephone with
*  
            Mr. C. Sizemore on November 21, 2007.
Maintenance Effectiveness Periodic Evaluation with Mr. Walt Smith,  
    *       Emergency Preparedness inspection with Ms. Ray and Mr. Tulley on
Acting Plant Manager on November 2, 2007.  
            December 13, 2007.
*  
    *       Occupational radiation safety cornerstone radiation monitoring instrumentation
Biennial Licensed Operator Requalification Program Inspection with  
            and protective equipment with Messrs. J. McCarthy and G. Packard and other
Mr. J. McCarthy on November 9, 2007.  
            licensee staff on December 14, 2007.
*  
ATTACHMENT: SUPPLEMENTAL INFORMATION
Overall assessments of the annual operating test via telephone with  
                                            49                                    Enclosure
Mr. C. Sizemore on November 21, 2007.  
*  
Emergency Preparedness inspection with Ms. Ray and Mr. Tulley on  
December 13, 2007.  
*  
Occupational radiation safety cornerstone radiation monitoring instrumentation  
and protective equipment with Messrs. J. McCarthy and G. Packard and other  
licensee staff on December 14, 2007.  
   
ATTACHMENT: SUPPLEMENTAL INFORMATION  


                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
1
Licensee
Attachment
R. Amundson, General Supervisor Operations Supervisor
SUPPLEMENTAL INFORMATION  
C. Butcher, Site Engineering Director
KEY POINTS OF CONTACT  
G. Casadonte, Fire Protection Coordinator
Licensee  
W. Godes, Training Supervisor
R. Amundson, General Supervisor Operations Supervisor  
R. Harrsch, Operations Manager
C. Butcher, Site Engineering Director  
M. Hayes, Radiation Protection Supervisor
G. Casadonte, Fire Protection Coordinator  
C. Jilek, Site Maintenance Rule Coordinator
W. Godes, Training Supervisor  
J. McCarthy, Site Vice-President
R. Harrsch, Operations Manager  
G. Packard, Plant Manager
M. Hayes, Radiation Protection Supervisor  
S. Pfaff, Performance Assessment Supervisor
C. Jilek, Site Maintenance Rule Coordinator  
K. Phillips, Outage Manager
J. McCarthy, Site Vice-President  
M. Ray, Regulatory Affairs Manager
G. Packard, Plant Manager  
C. Sizemore, Training Manager
S. Pfaff, Performance Assessment Supervisor
T. Schmitt, Lead health Physics Technician
K. Phillips, Outage Manager
S. Tulley, Emergency Preparedness Manager
M. Ray, Regulatory Affairs Manager  
B. Vandervelde, Maintenance Manager
C. Sizemore, Training Manager  
D. Villicana, Radiation Protection General Supervisor
T. Schmitt, Lead health Physics Technician
G. Young, Nuclear Oversight Manager
S. Tulley, Emergency Preparedness Manager  
Nuclear Regulatory Commission
B. Vandervelde, Maintenance Manager  
M. Kunowski, Chief, Reactor Projects, Branch 5
D. Villicana, Radiation Protection General Supervisor  
J. Cushing, Point Beach Project Manager, Office of Nuclear Reactor Regulation
G. Young, Nuclear Oversight Manager  
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened and Closed
Nuclear Regulatory Commission  
05000266/2007005-01;       FIN   Failure to Control Loose Materials Classified as Tornado
M. Kunowski, Chief, Reactor Projects, Branch 5  
05000301/2007005-01                Hazards (Section 1R01.1)
J. Cushing, Point Beach Project Manager, Office of Nuclear Reactor Regulation  
05000266/2007005-02;       FIN   Failure to Adequately Assess Operability of Service Water
05000301/2007005-02                Pump P-32C (Section 1R15.1)
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED  
05000301/2007005-03       NCV     Failure to Perform Operability Evaluations for Turbine-Driven
Opened and Closed  
                                  Auxiliary Feedwater Pump 2P-29 (Section 1R15.2)
05000266/2007005-01;  
05000266/2007005-04;       NCV   Failure to Have Adequate Procedures for the Refueling
05000301/2007005-01
05000301/2007005-04                Water Storage Tank (Section 4OA3.1)
FIN  
05000266/2007005-05;       NCV   Failure to Perform Adequate Post-Maintenance Testing for
Failure to Control Loose Materials Classified as Tornado  
05000301/2007005-05                the Turbine-Driven Auxiliary Feedwater Pumps
Hazards (Section 1R01.1)  
                                  (Section 4OA5.1)
05000266/2007005-02;  
                                                1                                    Attachment
05000301/2007005-02
FIN  
Failure to Adequately Assess Operability of Service Water  
Pump P-32C (Section 1R15.1)  
05000301/2007005-03  
NCV  
Failure to Perform Operability Evaluations for Turbine-Driven  
Auxiliary Feedwater Pump 2P-29 (Section 1R15.2)  
05000266/2007005-04;  
05000301/2007005-04
NCV  
Failure to Have Adequate Procedures for the Refueling  
Water Storage Tank (Section 4OA3.1)  
05000266/2007005-05;  
05000301/2007005-05
NCV  
Failure to Perform Adequate Post-Maintenance Testing for  
the Turbine-Driven Auxiliary Feedwater Pumps  
(Section 4OA5.1)  


05000301/2007005-06 NCV Failure to Adequately Evaluate a Condition Adverse to
                        Quality Associated with Turbine-Driven Auxiliary Feedwater
2
                        Pump 2P-29 (Section 4OA5.2.b.1)
Attachment
05000266/2007005-08; NCV Failure to Provide Adequate Guidance to Ensure the
05000301/2007005-06  
05000301/2007005-08      Operability of the MS System During a Steam Generator
NCV  
                        Tube Rupture. This Item was described in NRC Inspection
Failure to Adequately Evaluate a Condition Adverse to  
                        Report 2007301, dated August 21, 2007, as Item Numbers
Quality Associated with Turbine-Driven Auxiliary Feedwater  
                        05000266/2007301-01 and 05000301/2007301-01; however,
Pump 2P-29 (Section 4OA5.2.b.1)  
                        this item is being repeated in this table for NRC Plant Issues
05000266/2007005-08;  
                        Matrix tracking.
05000301/2007005-08
05000266/2007005-09; NCV Inadequate 10 CFR 72.48 Screening to Evaluate Possible
NCV  
05000301/2007005-09      Thermal Effects on Fuel Cladding (Section 4OA5.5)
Failure to Provide Adequate Guidance to Ensure the  
Opened
Operability of the MS System During a Steam Generator  
05000301/2007005-07 URI September 2007 Maintenance Activities Associated with
Tube Rupture. This Item was described in NRC Inspection  
                        Turbine-Driven Auxiliary Feedwater Pump 2P-29
Report 2007301, dated August 21, 2007, as Item Numbers  
                        (Section 4OA5.2.b.2)
05000266/2007301-01 and 05000301/2007301-01; however,  
Closed
this item is being repeated in this table for NRC Plant Issues  
05000266/2006011-01; VIO Failure to Update Final Safety Analysis Report with Reactor
Matrix tracking.  
05000301/2006011-01      Head Drop Analysis and Obtain NRC Approval
05000266/2007005-09;  
                        (Section 4OA3.2)
05000301/2007005-09
05000266/2006004-05; URI Inadequate 10 CFR 72.48 Screening to Evaluate Possible
NCV  
05000301/2006004-05      Thermal Effects on Fuel Cladding (Section 4OA5.5)
Inadequate 10 CFR 72.48 Screening to Evaluate Possible  
07200005/2004003-01 URI Adequacy of Design Calculation, PBNP-305336-SO1
Thermal Effects on Fuel Cladding (Section 4OA5.5)  
                        (Section 4OA5.6)
                                        2                                    Attachment
Opened  
05000301/2007005-07  
URI  
September 2007 Maintenance Activities Associated with  
Turbine-Driven Auxiliary Feedwater Pump 2P-29  
(Section 4OA5.2.b.2)  
Closed  
05000266/2006011-01;  
05000301/2006011-01
VIO  
Failure to Update Final Safety Analysis Report with Reactor  
Head Drop Analysis and Obtain NRC Approval  
(Section 4OA3.2)  
05000266/2006004-05;  
05000301/2006004-05
URI  
Inadequate 10 CFR 72.48 Screening to Evaluate Possible  
Thermal Effects on Fuel Cladding (Section 4OA5.5)  
07200005/2004003-01  
URI  
Adequacy of Design Calculation, PBNP-305336-SO1  
(Section 4OA5.6)  


                                  LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
3
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
Attachment
selected sections or portions of the documents were evaluated as part of the overall inspection
LIST OF DOCUMENTS REVIEWED  
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
The following is a partial list of documents reviewed during the inspection. Inclusion on this list  
any part of it, unless this is stated in the body of the inspection report.
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that  
1R01 Adverse Weather Protection
selected sections or portions of the documents were evaluated as part of the overall inspection  
Issue Reports:
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
- CAP 01114731; Loose Materials Found in the Protected Area; October 19, 2007
any part of it, unless this is stated in the body of the inspection report.  
- CAP 01114637; Material in Yard; 10/18/2007
- CAP 01094135; Tornado Hazards Identified Performing PC 99; May 25, 2007
1R01 Adverse Weather Protection
- CAP 01102551; Tornado Hazards Identified Performing PC-99; July 19, 2007
Issue Reports:  
- CAP 01112508; Tornado hazards Identified Performing PC-99; September 21, 2007
- CAP 01114731; Loose Materials Found in the Protected Area; October 19, 2007  
- CAP 01098214; 3 or More Tornado Hazards in Single Inspection. Area; June 21, 2007
- CAP 01114637; Material in Yard; 10/18/2007  
Procedures:
- CAP 01094135; Tornado Hazards Identified Performing PC 99; May 25, 2007  
- PC 99; Tornado Hazards Inspection Checklist; Revision 0
- CAP 01102551; Tornado Hazards Identified Performing PC-99; July 19, 2007  
- AOP-13C; Severe Weather Conditions; Revision 17
- CAP 01112508; Tornado hazards Identified Performing PC-99; September 21, 2007  
- NP 1.9.6; Plant Cleanliness and Storage; Revision 22
- CAP 01098214; 3 or More Tornado Hazards in Single Inspection. Area; June 21, 2007  
1R04 Equipment Alignment
Procedures:  
- CL 11A G01; G01 Emergency Diesel Generator Checklist; Revision 22
- PC 99; Tornado Hazards Inspection Checklist; Revision 0  
- CL 11A G02; G02 Emergency Diesel Generator Checklist; Revision 26
- AOP-13C; Severe Weather Conditions; Revision 17  
- CL 13, Part 1; Auxiliary Feedwater Lineup Unit 1 Turbine Driven; Revision 36
- NP 1.9.6; Plant Cleanliness and Storage; Revision 22  
- CL 13, Part 1; Auxiliary Feedwater Lineup Unit 2 Turbine Driven; Revision 40
1R04 Equipment Alignment
- CL 13, Part 1; Auxiliary Feedwater Lineup Motor Driven; Revision 42
- CL 11A G01; G01 Emergency Diesel Generator Checklist; Revision 22  
- O-SOP-G01-001; Maintenance Operation for Emergency Diesel Generator G01; Revision 5
- CL 11A G02; G02 Emergency Diesel Generator Checklist; Revision 26  
- O-SOP-G01-002; Maintenance Operation for Emergency Diesel Generator G02; Revision 8
- CL 13, Part 1; Auxiliary Feedwater Lineup Unit 1 Turbine Driven; Revision 36  
- O-TS-AFW-002; Auxiliary Feedwater System Valve and Lock Checklist - Monthly; Revision 10
- CL 13, Part 1; Auxiliary Feedwater Lineup Unit 2 Turbine Driven; Revision 40  
1R05 Fire Protection
- CL 13, Part 1; Auxiliary Feedwater Lineup Motor Driven; Revision 42  
Fire Hazards Analysis Report; January 2007 Revision
- O-SOP-G01-001; Maintenance Operation for Emergency Diesel Generator G01; Revision 5  
1R07 Heat Sink Performance
- O-SOP-G01-002; Maintenance Operation for Emergency Diesel Generator G02; Revision 8  
Documents:
- O-TS-AFW-002; Auxiliary Feedwater System Valve and Lock Checklist - Monthly; Revision 10  
- Bio/Silt Fouling Inspection Form for EDG G01 Heat Exchanger; November 2007
1R05 Fire Protection
- Bio/Silt Fouling Inspection Form for EDG G02 Heat Exchanger; December 2007
Fire Hazards Analysis Report; January 2007 Revision  
1R11 Licensed Operator Requalification Program
1R07 Heat Sink Performance
Issued Reports:
Documents:  
- Point Beach ROP Plant Issue Matrix from 09/01/2005 to 10/11/2007; October 11, 2007
- Bio/Silt Fouling Inspection Form for EDG G01 Heat Exchanger; November 2007  
- Point Beach Nuclear Plant, Units 1 and 2 NRC Integrated Inspection Reports; dated various
- Bio/Silt Fouling Inspection Form for EDG G02 Heat Exchanger; December 2007  
  from October 26, 2005, through October 26, 2007
1R11 Licensed Operator Requalification Program
                                                    3                                  Attachment
Issued Reports:  
- Point Beach ROP Plant Issue Matrix from 09/01/2005 to 10/11/2007; October 11, 2007  
- Point Beach Nuclear Plant, Units 1 and 2 NRC Integrated Inspection Reports; dated various  
from October 26, 2005, through October 26, 2007  


- LER 266/2005-007-00; Control Rod Movement With Refueling Cavity Water Level Below
  TS 3.9.6 Limit; January 16, 2006
4
- Nuclear Oversight Assessment Reports for Point Beach; dated various 2006 and 2007
Attachment
- Operations Training Advisory Committee Meeting Minutes; dated various from
- LER 266/2005-007-00; Control Rod Movement With Refueling Cavity Water Level Below  
  March 15, 2006, through September 13, 2007
TS 3.9.6 Limit; January 16, 2006  
- LOR Curriculum Review Committee Meeting Minutes; dated various from March 7, 2006,
- Nuclear Oversight Assessment Reports for Point Beach; dated various 2006 and 2007  
  through September 28, 2007
- Operations Training Advisory Committee Meeting Minutes; dated various from  
- AO Curriculum Review Committee Meeting Minutes; February 21, 2007
March 15, 2006, through September 13, 2007  
- Completed TRQM 19.32; Activation of an Inactive SRO License; Two Separate Forms;
- LOR Curriculum Review Committee Meeting Minutes; dated various from March 7, 2006,  
  February 24, 2006, and June 5, 2006
through September 28, 2007  
- Completed PBF-2094; NRC License Active Status Tracking; dated various
- AO Curriculum Review Committee Meeting Minutes; February 21, 2007  
- Completed PBF-6097; Operations Watchstander Temporary Restriction Form; dated various
- Completed TRQM 19.32; Activation of an Inactive SRO License; Two Separate Forms;  
- Licensed Operator Quarterly Status Report; dated various
February 24, 2006, and June 5, 2006  
- Operations Continuing Training End of Cycle Reports; dated various 2006 and 2007
- Completed PBF-2094; NRC License Active Status Tracking; dated various  
- QF-1050-01a; Course/Cycle Feedback Summary Form; dated various 2006 and 2007
- Completed PBF-6097; Operations Watchstander Temporary Restriction Form; dated various  
- 2007 - 2008 LOR Biennial Training Plan (BTP); Revision 3
- Licensed Operator Quarterly Status Report; dated various  
- 2006 NRC Biennial Written Exams; dated various
- Operations Continuing Training End of Cycle Reports; dated various 2006 and 2007  
- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Summary
- QF-1050-01a; Course/Cycle Feedback Summary Form; dated various 2006 and 2007  
- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Test Item Statistics
- 2007 - 2008 LOR Biennial Training Plan (BTP); Revision 3  
- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Sample Plan
- 2006 NRC Biennial Written Exams; dated various  
- Evaluation ID# PB-LOR-006-001E; Written Exam Item Review; August 6, 2007
- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Summary  
- Management Observations of Training 2006 and 2007
- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Test Item Statistics  
- Licensee 71111.11 Pre-Inspection; August 13, 2007
- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Sample Plan  
- LOR Cycle Attendance Sheets; dated various
- Evaluation ID# PB-LOR-006-001E; Written Exam Item Review; August 6, 2007  
- Completed QF-1040-04; Remediation Training Form; dated various
- Management Observations of Training 2006 and 2007  
- Completed QF-1040-15; Self-Study/Make-Up Training Form; dated various
- Licensee 71111.11 Pre-Inspection; August 13, 2007  
- Completed QF-1073-01; Walkthrough Exam Summary; Exam Weeks 5 and 6 of 2007; dated
- LOR Cycle Attendance Sheets; dated various  
  various
- Completed QF-1040-04; Remediation Training Form; dated various  
- Completed QF-1073-02; Crew Simulator Evaluation Summary; Exam Weeks 5 and 6 of 2007;
- Completed QF-1040-15; Self-Study/Make-Up Training Form; dated various  
  dated various
- Completed QF-1073-01; Walkthrough Exam Summary; Exam Weeks 5 and 6 of 2007; dated  
- Completed QF-1073-03; Individual Operator Simulator Examination Summary; Exam Weeks 5
various  
  and 6 of 2007; dated various
- Completed QF-1073-02; Crew Simulator Evaluation Summary; Exam Weeks 5 and 6 of 2007;  
- Completed QF-1073-04; Remediation Training Form; Exam Weeks 5 and 6 of 2007; dated
dated various  
  various
- Completed QF-1073-03; Individual Operator Simulator Examination Summary; Exam Weeks 5  
- Simulator Review Committee Meeting Minutes; dated various from March 2, 2006, through
and 6 of 2007; dated various  
  September 13, 2007
- Completed QF-1073-04; Remediation Training Form; Exam Weeks 5 and 6 of 2007; dated  
- FP-T-SAT-81; Simulator Testing and Documentation; Revision 4
various  
- SWO 05-0039; Rehost Simulator PPCS, March 22, 2005
- Simulator Review Committee Meeting Minutes; dated various from March 2, 2006, through  
- SIMGL C1.4; Install and Test U1C31; November 2, 2007
September 13, 2007  
- SIMGL C3.3; Simulator Certification Testing; September 21, 2005
- FP-T-SAT-81; Simulator Testing and Documentation; Revision 4  
- SCT 6.8.37.5; Stuck Open Condenser Dump Valve; August 29, 2006
- SWO 05-0039; Rehost Simulator PPCS, March 22, 2005  
- SCT 6.3.2; 75 Percent Power Heat Balance; July 12, 2006
- SIMGL C1.4; Install and Test U1C31; November 2, 2007  
- SCT 6.1.4; 100 Percent Steady State Drift Test; July 11, 2006
- SIMGL C3.3; Simulator Certification Testing; September 21, 2005  
- SCT 6.8.13.3; Loss of a 4160 Volt Bus; December 7, 2006
- SCT 6.8.37.5; Stuck Open Condenser Dump Valve; August 29, 2006  
- SCT 6.8.16.3; Generator Inadvertent Trip; July 18, 2006
- SCT 6.3.2; 75 Percent Power Heat Balance; July 12, 2006  
- SCT 6.5.1; Manual Reactor Trip; April 3, 2006
- SCT 6.1.4; 100 Percent Steady State Drift Test; July 11, 2006  
- SCT 6.5.8; Loss of Coolant Accident With Loss of Offsite Power; March 30, 2006
- SCT 6.8.13.3; Loss of a 4160 Volt Bus; December 7, 2006  
- Simulator Review Committee Meeting Minutes; June 28, 2007
- SCT 6.8.16.3; Generator Inadvertent Trip; July 18, 2006  
- Simulator Review Committee Meeting Minutes; February 12, 2007
- SCT 6.5.1; Manual Reactor Trip; April 3, 2006  
- Simulator Work Orders Closed Out in Previous 12 Months; November 1, 2007
- SCT 6.5.8; Loss of Coolant Accident With Loss of Offsite Power; March 30, 2006  
- List of Open Simulator SWOs; November 1, 2007
- Simulator Review Committee Meeting Minutes; June 28, 2007  
                                                4                                Attachment
- Simulator Review Committee Meeting Minutes; February 12, 2007  
- Simulator Work Orders Closed Out in Previous 12 Months; November 1, 2007  
- List of Open Simulator SWOs; November 1, 2007  


- FP-T-SAT-80; Simulator Configuration Management; September 28, 2007
- FP-T-SAT-81; Simulator Testing and Documentation; September 28, 2007
5
- SIMGL C3.3; Simulator Certification Testing; September 21, 2005
Attachment
- SIMGL C1.4; Simulator Modifications and Core Load Changes (Completed for Unit 1);
- FP-T-SAT-80; Simulator Configuration Management; September 28, 2007  
  November 2, 2007
- FP-T-SAT-81; Simulator Testing and Documentation; September 28, 2007  
- ANSI/ANS-3.5-1985; Nuclear Power Plant Simulators for Use in Operator Training;
- SIMGL C3.3; Simulator Certification Testing; September 21, 2005  
  October 25, 1985
- SIMGL C1.4; Simulator Modifications and Core Load Changes (Completed for Unit 1);  
- Regulatory Guide 1.149; Nuclear Power Plant Simulation Facilities for Use in Operator License
November 2, 2007  
  Examinations; Revision 1; April 1987
- ANSI/ANS-3.5-1985; Nuclear Power Plant Simulators for Use in Operator Training;  
- ANSI/ANS-3.4-1996; Medical Certification and Monitoring of Personnel Requiring Operator
October 25, 1985
  Licenses for Nuclear Power Plants; February 7, 1996
- Regulatory Guide 1.149; Nuclear Power Plant Simulation Facilities for Use in Operator License  
- Regulatory Guide 1.134; Medical Evaluation of Licensed Personnel for Nuclear Power Plants;
Examinations; Revision 1; April 1987  
  Revision 3; March 1998
- ANSI/ANS-3.4-1996; Medical Certification and Monitoring of Personnel Requiring Operator  
- Seven Licensed Operators Medical Records; dated various
Licenses for Nuclear Power Plants; February 7, 1996  
- TRR 01116172; Review Two Exam Bank Questions for Difficulty Level Changes;
- Regulatory Guide 1.134; Medical Evaluation of Licensed Personnel for Nuclear Power Plants;  
  November 8, 2007
Revision 3; March 1998  
- TRR 01116174; Review Two JPMs for Difficulty Level; November 8, 2007
- Seven Licensed Operators Medical Records; dated various  
Procedures:
- TRR 01116172; Review Two Exam Bank Questions for Difficulty Level Changes;  
- FP-T-SAT-73; Licensed Operator Requalification Program Examinations; Revision 2
November 8, 2007  
- JPM P000.042bAOT; Lineup for Transfer to Containment Sump Post-Accident Recirculation;
- TRR 01116174; Review Two JPMs for Difficulty Level; November 8, 2007  
  Revision 4
Procedures:  
- SEG # PB-LOR-07E-001S; High Impact Session - PZR Pressure Transmitter RTS,
- FP-T-SAT-73; Licensed Operator Requalification Program Examinations; Revision 2  
  EH Malfunction and Containment Sump Recirculation; Revision 0
- JPM P000.042bAOT; Lineup for Transfer to Containment Sump Post-Accident Recirculation;  
- EOP-1.3 Unit 1; Transfer to Containment Sump Recirculation - Low Head Injection;
Revision 4  
  Revision 39
- SEG # PB-LOR-07E-001S; High Impact Session - PZR Pressure Transmitter RTS,  
- FL-LOR-TPD; NMC Fleet Licensed Operator Requalification Training Program Description;
EH Malfunction and Containment Sump Recirculation; Revision 0  
  Revision 0
- EOP-1.3 Unit 1; Transfer to Containment Sump Recirculation - Low Head Injection;  
- TRPR 33.0; Training Program Description; Licensed Operator Requalification Training
Revision 39  
  Program; Revision 25
- FL-LOR-TPD; NMC Fleet Licensed Operator Requalification Training Program Description;  
- OM 3.10; Operations Personnel Assignments and Scheduling; Revision 23; August 9, 2007
Revision 0  
- FP-T-SAT-71; NRC Examination Security Requirements; Revision 0
- TRPR 33.0; Training Program Description; Licensed Operator Requalification Training  
- CAP 01040650; Simulator PPCS Failed Completely, Affecting LOR As Found; July 20, 2006
Program; Revision 25  
- CAP 01073895; EP Issues from LOR 2006 Annual Operating Exams; January 25, 2007
- OM 3.10; Operations Personnel Assignments and Scheduling; Revision 23; August 9, 2007  
- CAP 01092718; LOR Cycle 07C Schedule Affected by Simulator Malfunctions; May 15, 2007
- FP-T-SAT-71; NRC Examination Security Requirements; Revision 0  
- CAP 01111841; RWST Temp Found High OOS on Logs; September 18, 2007
- CAP 01040650; Simulator PPCS Failed Completely, Affecting LOR As Found; July 20, 2006  
- CAP 01113938; Operations Quarterly Status Report Accuracy Questioned; October 9, 2007
- CAP 01073895; EP Issues from LOR 2006 Annual Operating Exams; January 25, 2007  
- CAP 01115710; Annual Operating Exam Security Lapse Results in Rework;
- CAP 01092718; LOR Cycle 07C Schedule Affected by Simulator Malfunctions; May 15, 2007  
  November 1, 2007
- CAP 01111841; RWST Temp Found High OOS on Logs; September 18, 2007  
- NP 1.10.1; Record Keeping for NRC Licensed Operators; July 20, 2005
- CAP 01113938; Operations Quarterly Status Report Accuracy Questioned; October 9, 2007  
- OM 4.3.2; EOP/AOP Verification/Validation Process; Revision 15; October 29, 2007
- CAP 01115710; Annual Operating Exam Security Lapse Results in Rework;  
CAPs/PCRs/TRRs Initiated for NRC-Identified Issues:
November 1, 2007  
- CAP 01115978; Watchstander Restriction Form Not Filled Out Correctly; November 7, 2007
- NP 1.10.1; Record Keeping for NRC Licensed Operators; July 20, 2005  
- CAP 01116144; PCRs Generated from CDBI Closed Out With No Action Taken;
- OM 4.3.2; EOP/AOP Verification/Validation Process; Revision 15; October 29, 2007  
  November 8, 2007
CAPs/PCRs/TRRs Initiated for NRC-Identified Issues:  
- CAP 01116160; Simulator PPCS Problems During Exams; November 8, 2007
- CAP 01115978; Watchstander Restriction Form Not Filled Out Correctly; November 7, 2007  
- PCR 01116095; Revise EOP 1.3 Unit 1; November 8, 2007
- CAP 01116144; PCRs Generated from CDBI Closed Out With No Action Taken;  
- PCR 01116097; Revise EOP 1.3 Unit 2; November 8, 2007
November 8, 2007  
                                                5                                  Attachment
- CAP 01116160; Simulator PPCS Problems During Exams; November 8, 2007  
- PCR 01116095; Revise EOP 1.3 Unit 1; November 8, 2007  
- PCR 01116097; Revise EOP 1.3 Unit 2; November 8, 2007  


1R13 Maintenance Risk Assessments and Emergent Work Control
- NP 10.3.6; Shutdown Safety Review and Safety Assessment; Revision 19
6
- Safety Monitor Calculation Reports for Units 1 and 2 for Applicable Work Weeks
Attachment
- Work Week Execution Schedules for the Applicable Work Weeks
1R13 Maintenance Risk Assessments and Emergent Work Control
- Operator Logs for the Applicable Work Weeks
- NP 10.3.6; Shutdown Safety Review and Safety Assessment; Revision 19  
1R15 Operability Evaluations
- Safety Monitor Calculation Reports for Units 1 and 2 for Applicable Work Weeks  
Issue Reports:
- Work Week Execution Schedules for the Applicable Work Weeks  
- CAP 01111251; Discrepancy in CAF BHP Measured vs. Vendor Data; September 13, 2007
- Operator Logs for the Applicable Work Weeks  
- OPR 154; Overload Concerns of Safeguards 480V AC Load Control and Motor Control
1R15 Operability Evaluations
  Centers; Revisions 1 Through 3
Issue Reports:  
- OPR 157; EDG Operability Related to Electrical Loading During Certain Accident Scenarios;
- CAP 01111251; Discrepancy in CAF BHP Measured vs. Vendor Data; September 13, 2007  
  Revision 3
- OPR 154; Overload Concerns of Safeguards 480V AC Load Control and Motor Control  
- AR 01106938-01; Past Operability of P-32C; 10/25/2007
Centers; Revisions 1 Through 3  
- CAP 01098680; P-32C SW Pump Vibration Nearing Acceptance Criteria Limit; June 24, 2007
- OPR 157; EDG Operability Related to Electrical Loading During Certain Accident Scenarios;  
- OPR 01098680; P-32C, Service Water Pump; Revision 0
Revision 3  
- ACE 01098680-02; P-32C Vibration Issues; October 5, 2007
- AR 01106938-01; Past Operability of P-32C; 10/25/2007  
- CAP 01105929; P-32C SW Pump Fails IT-07C Testing; August 8, 2007
- CAP 01098680; P-32C SW Pump Vibration Nearing Acceptance Criteria Limit; June 24, 2007  
- CAP 01114171; OI 35C Requires Extensive Rewriting; October 11, 2007
- OPR 01098680; P-32C, Service Water Pump; Revision 0  
- CAP 01119241; Concerns of PBNPs Use of IST Trend Data in OPRs; January 4, 2008
- ACE 01098680-02; P-32C Vibration Issues; October 5, 2007
- CAP 01112660, 2P-29 Outboard Bearing Water Following IT-09A; September 24, 2007
- CAP 01105929; P-32C SW Pump Fails IT-07C Testing; August 8, 2007  
- CAP 01113318, IT-09A Oil Analysis Results Not As Expected for 2P-29; September 27, 2007
- CAP 01114171; OI 35C Requires Extensive Rewriting; October 11, 2007  
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 2,
- CAP 01119241; Concerns of PBNPs Use of IST Trend Data in OPRs; January 4, 2008  
  November 3, 2007
- CAP 01112660, 2P-29 Outboard Bearing Water Following IT-09A; September 24, 2007  
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 3,
- CAP 01113318, IT-09A Oil Analysis Results Not As Expected for 2P-29; September 27, 2007  
  November 4, 2007
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 2,  
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 4,
November 3, 2007  
  November 7, 2007
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 3,  
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 5,
November 4, 2007  
  November 10, 2007
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 4,  
Procedures:
November 7, 2007  
- OI-35C; 480V Electrical Load Conservation; Revisions 3 and 4
- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 5,  
- IT-07C; P-32C Service Water Pump (Quarterly); Revision 18
November 10, 2007  
1R17 Permanent Plant Modifications
Procedures:  
- Engineering Modification 05-006 and Engineering Changes EC1590 and 1591 Associated
- OI-35C; 480V Electrical Load Conservation; Revisions 3 and 4  
  With the Replacement of the EDG Heat Exchangers for EDGs G01 and G02
- IT-07C; P-32C Service Water Pump (Quarterly); Revision 18  
1R19 Post-Maintenance Testing
1R17 Permanent Plant Modifications  
Procedures:
- Engineering Modification 05-006 and Engineering Changes EC1590 and 1591 Associated  
- RMP 9216-5;Service Water Pump Bowl Assembly Inspection and Maintenance; Revision 3
With the Replacement of the EDG Heat Exchangers for EDGs G01 and G02  
- IT 07E; P-32E Service Water Pump (Quarterly); Revision 19
1R19 Post-Maintenance Testing
- RMP 9387; AC Induction Motor MCE Testing Procedure; Revision 4
Procedures:  
- IT-21; Charging Pumps and Valves Quarterly; Revision 18
- RMP 9216-5;Service Water Pump Bowl Assembly Inspection and Maintenance; Revision 3  
- RMP 9003-1; Charging Pump Overhaul; Revision 6
- IT 07E; P-32E Service Water Pump (Quarterly); Revision 19  
                                                6                                Attachment
- RMP 9387; AC Induction Motor MCE Testing Procedure; Revision 4  
- IT-21; Charging Pumps and Valves Quarterly; Revision 18  
- RMP 9003-1; Charging Pump Overhaul; Revision 6  


Work Orders:
- WO 302859-01; Service Water Pump Maintenance; October 24, 2007
7
- WO 300182-02; P-32E Service Water Pump Lower Than Expected Insul Resistance Reading;
Attachment
  October 24, 2007
Work Orders:  
- WO 219880; CVCS Charging Pump Modification - Pump 1P2B Renovation; Revision 0
- WO 302859-01; Service Water Pump Maintenance; October 24, 2007  
1R22 Surveillance Testing
- WO 300182-02; P-32E Service Water Pump Lower Than Expected Insul Resistance Reading;  
Procedures:
October 24, 2007  
- IT-65; Containment Isolation Valves Quarterly; Revision 35
- WO 219880; CVCS Charging Pump Modification - Pump 1P2B Renovation; Revision 0  
- PBTP 158; Leak rate Testing of 2SC-966C Containment Isolation Valve at Power; Revision 0
1R22 Surveillance Testing
- IT-09A; Cold Start of the Turbine Driven Auxiliary Feedwater Pump Unit 2; Revision 45
Procedures:  
- TS-81; Emergency Diesel Generator G01; Revision 75
- IT-65; Containment Isolation Valves Quarterly; Revision 35  
- TS-82; Emergency Diesel Generator G02; Revision 76
- PBTP 158; Leak rate Testing of 2SC-966C Containment Isolation Valve at Power; Revision 0  
1R23 Temporary Plant Modifications
- IT-09A; Cold Start of the Turbine Driven Auxiliary Feedwater Pump Unit 2; Revision 45  
Engineering Change:
- TS-81; Emergency Diesel Generator G01; Revision 75  
- EC11633; Furmanite Injection of 2MS-232A MSR Valve
- TS-82; Emergency Diesel Generator G02; Revision 76  
Work Orders:
1R23 Temporary Plant Modifications
- WO 340064; Furmanite Injection of 2MS-232A MSR Valve
Engineering Change:  
- WO 346804; Furmanite Injection of 2MS-232A MSR Valve
- EC11633; Furmanite Injection of 2MS-232A MSR Valve  
2OS3 Radiation Monitoring Instrumentation and Protective Equipment
Work Orders:  
Issue Reports:
- WO 340064; Furmanite Injection of 2MS-232A MSR Valve  
- Point Beach Nuclear Plant Radiation Monitoring System Health Report; December 6, 2007
- WO 346804; Furmanite Injection of 2MS-232A MSR Valve  
- Snapshot Self-Assessment Report; SCBA Maintenance and User Training;
2OS3 Radiation Monitoring Instrumentation and Protective Equipment
  November 30, 2007
Issue Reports:  
- Snapshot Self-Assessment Report; IP 71121.03 Inspection; November 30, 2007
- Point Beach Nuclear Plant Radiation Monitoring System Health Report; December 6, 2007
- Snapshot Self-Assessment Report; 2006 INPO Area for Improvement - Radiation Monitoring
- Snapshot Self-Assessment Report; SCBA Maintenance and User Training;  
  Instrument Program; November 23, 2007
November 30, 2007  
- Radiation Protection Instrument Inventory and Calibration Due Date Report;
- Snapshot Self-Assessment Report; IP 71121.03 Inspection; November 30, 2007  
  December 7, 2007
- Snapshot Self-Assessment Report; 2006 INPO Area for Improvement - Radiation Monitoring  
Instrument Program; November 23, 2007  
- Radiation Protection Instrument Inventory and Calibration Due Date Report;  
December 7, 2007  
- Radcal Corporation Certificate of Conformance for Electrometer/Ion Chamber Model 20-X5-
- Radcal Corporation Certificate of Conformance for Electrometer/Ion Chamber Model 20-X5-
  1800 (SN 21707), Model 20X5-3 (SN 21548) and Model 20-X5-60 (SN 21344);
1800 (SN 21707), Model 20X5-3 (SN 21548) and Model 20-X5-60 (SN 21344);  
  September 21, 2005
September 21, 2005
- Report of Calibration for the Canberra Fastscan Whole Body Count System at the Point Beach
- Report of Calibration for the Canberra Fastscan Whole Body Count System at the Point Beach  
  Nuclear Plant; January 26, 2007
Nuclear Plant; January 26, 2007
- Report of Evaluation of Isotopic Mixture and RP Programs; January 31, 2007
- Report of Evaluation of Isotopic Mixture and RP Programs; January 31, 2007  
- Calibration Record for MGP Instrument Model AMP-100 (SN 474103); March 24, 2007
- Calibration Record for MGP Instrument Model AMP-100 (SN 474103); March 24, 2007  
- Calibration Record for Eberline Instrument Model AMS-4 (SN A021); January 27, 2007
- Calibration Record for Eberline Instrument Model AMS-4 (SN A021); January 27, 2007  
- Point Beach Emergency Plan Manual; EP 7.0 - Emergency Facilities and Equipment;
- Point Beach Emergency Plan Manual; EP 7.0 - Emergency Facilities and Equipment;  
  Revision 51
Revision 51  
- Qualification Matrix and Training Status for Respiratory Protection; December 11, 2007
- Qualification Matrix and Training Status for Respiratory Protection; December 11, 2007  
- Lesson Plan No. PB-SHE-004-SCRL; Respiratory Protection; Revision 1
- Lesson Plan No. PB-SHE-004-SCRL; Respiratory Protection; Revision 1  
- Scott Posicheck 3; Visual and Functional Test Records for Point Beach SCBA Units;
- Scott Posicheck 3; Visual and Functional Test Records for Point Beach SCBA Units;  
  March 20, 2007
March 20, 2007  
                                                7                                  Attachment


Procedures:
- HPIP 7.52.4; PM-7 Personnel Monitor Checks; Revision 12
8
- HPIP 7.52.1; Personnel Contamination Monitor (PCM-1B/1C) Source Response Check;
Attachment
  Revision 13
Procedures:  
- HPIP 5.66; Functional Check of the Gamma-60 Portal Monitor; Revision 21
- HPIP 7.52.4; PM-7 Personnel Monitor Checks; Revision 12  
- HPIP 2.1.1; Response Checks of Portable Survey Instruments; Revision 9
- HPIP 7.52.1; Personnel Contamination Monitor (PCM-1B/1C) Source Response Check;  
- HPIP 1.74; Operation of the Canberra Whole Body Counter; Revision 7
Revision 13  
- HPCAL 3.2; Area Monitor Calibration Procedure DA1-1 and DA1-6 Detector Assemblies and
- HPIP 5.66; Functional Check of the Gamma-60 Portal Monitor; Revision 21  
  Associated Calibration Records for Unit 1 and Unit 2 Charging Pump Room (Low Range)
- HPIP 2.1.1; Response Checks of Portable Survey Instruments; Revision 9  
  ARMs; December 19, 2006, and September 15, 2006
- HPIP 1.74; Operation of the Canberra Whole Body Counter; Revision 7  
- HPCAL 3.3; Area Monitor Calibration Procedure DA1-4 and DA1-5 Detector Assemblies and
- HPCAL 3.2; Area Monitor Calibration Procedure DA1-1 and DA1-6 Detector Assemblies and  
  Associated Calibration Records for Unit 1 and Unit 2 Charging Pump Room (High Range)
Associated Calibration Records for Unit 1 and Unit 2 Charging Pump Room (Low Range)  
  ARMs; February 15, 2007, and February 12, 2007
ARMs; December 19, 2006, and September 15, 2006
- HPCAL 3.2 Calibration Record for Unit 1 and Unit 2 Seal Table ARMs; April 1, 2007, and
- HPCAL 3.3; Area Monitor Calibration Procedure DA1-4 and DA1-5 Detector Assemblies and  
  October 15, 2006
Associated Calibration Records for Unit 1 and Unit 2 Charging Pump Room (High Range)  
- HPCAL 3.2 Calibration Record for Unit 1 and Unit 2 Post Accident Sample Line Monitors;
ARMs; February 15, 2007, and February 12, 2007  
  August 13, 2007, and April 17, 2007
- HPCAL 3.2 Calibration Record for Unit 1 and Unit 2 Seal Table ARMs; April 1, 2007, and  
- HP CAL 3.2 Calibration Record for Safety Injection Pump Room Low Range and High Range
October 15, 2006  
  ARMs; September 18, 2006, and July 17, 2006
- HPCAL 3.2 Calibration Record for Unit 1 and Unit 2 Post Accident Sample Line Monitors;  
- 2ICP 13.017; Containment High Range Radiation Monitoring System Channels 2RE126,
August 13, 2007, and April 17, 2007  
  2RE127, 2RE128 Calibration; December 12, 2006
- HP CAL 3.2 Calibration Record for Safety Injection Pump Room Low Range and High Range  
- 1ICP 13.017; Containment High Range Radiation Monitoring System Channels 1RE126,
ARMs; September 18, 2006, and July 17, 2006  
  1RE127, 1RE-128 Calibration; March 14, 2007
- 2ICP 13.017; Containment High Range Radiation Monitoring System Channels 2RE126,  
- HPCAL 3.11; Containment High Range Detector Response Check Surveillance Record, Unit 1
2RE127, 2RE128 Calibration; December 12, 2006  
  Detectors (1RE126, 127 and 128), April 11, 2007; and Unit 2 Detectors (2RE126, 127 and
- 1ICP 13.017; Containment High Range Radiation Monitoring System Channels 1RE126,  
  128), October 16, 2006
1RE127, 1RE-128 Calibration; March 14, 2007  
- HPCAL 1.10.2; Verification of J.L. Shepherd Model 89 Calibrator Dose Rates (Revision 1) and
- HPCAL 3.11; Containment High Range Detector Response Check Surveillance Record, Unit 1  
  Associated Output Verification for Calibrator No. 8269 and No. 8228; September 28, 2006
Detectors (1RE126, 127 and 128), April 11, 2007; and Unit 2 Detectors (2RE126, 127 and  
- HPCAL 1.1; Portable Survey Instrument Calibration, Repair and Response Checks;
128), October 16, 2006
  Revision 18
- HPCAL 1.10.2; Verification of J.L. Shepherd Model 89 Calibrator Dose Rates (Revision 1) and  
- NMC Fleet Procedure FP-RP-ICC-01; Instrument Control and Calibration/Functional Testing
Associated Output Verification for Calibrator No. 8269 and No. 8228; September 28, 2006
  Frequencies of RP Instruments; Revision 3
- HPCAL 1.1; Portable Survey Instrument Calibration, Repair and Response Checks;  
- HPCAL 1.38; Calibration of the Portable Neutron Survey Instrument Analog Smart Portable
Revision 18  
  (ASP-1), and Associated Calibration Record (Instrument No. 9459); March 9, 2007
- NMC Fleet Procedure FP-RP-ICC-01; Instrument Control and Calibration/Functional Testing  
- HPCAL 2.8; Eberline PCM-1B Personnel Contamination Monitor Calibration Procedure and
Frequencies of RP Instruments; Revision 3
  Associated Calibration Record for Monitor No. 7737, October 17, 2007; No.7738,
- HPCAL 1.38; Calibration of the Portable Neutron Survey Instrument Analog Smart Portable  
  March 30, 2007; and No. 7739, May 8, 2007
(ASP-1), and Associated Calibration Record (Instrument No. 9459); March 9, 2007  
- HPCAL 2.8.1; Personnel Contamination Monitor Detector Efficiency Determination and
- HPCAL 2.8; Eberline PCM-1B Personnel Contamination Monitor Calibration Procedure and  
  Associated Record for Monitor No. 7739; July 13, 2007
Associated Calibration Record for Monitor No. 7737, October 17, 2007; No.7738,  
- HPCAL 2.11.1; Calibration of the Gamma-60 Portal Monitor and Associated Calibration
March 30, 2007; and No. 7739, May 8, 2007  
  Record for Monitor No. 9485, March 12, 2007; and No. 9486, February 22, 2007
- HPCAL 2.8.1; Personnel Contamination Monitor Detector Efficiency Determination and  
- HPCAL 2.21; Calibration of the Eberline Personnel Monitor PM-7 and Associated Calibration
Associated Record for Monitor No. 7739; July 13, 2007  
  Record for Monitor No. A112 (November 28, 2007); No. A113 (October 29, 2007); and
- HPCAL 2.11.1; Calibration of the Gamma-60 Portal Monitor and Associated Calibration  
  No. A114; (September 21, 2007)
Record for Monitor No. 9485, March 12, 2007; and No. 9486, February 22, 2007
- HPCAL 2.15; Small Articles Monitor Type SAM 9/11 Calibration and Efficiency and Associated
- HPCAL 2.21; Calibration of the Eberline Personnel Monitor PM-7 and Associated Calibration  
  Calibration Record for Monitor No. 2; September 26, 2007
Record for Monitor No. A112 (November 28, 2007); No. A113 (October 29, 2007); and  
- PC 75 Part 1; Monthly and Turnaround Maintenance for the Scott Model 4.5 Self-Contained
No. A114; (September 21, 2007)  
  Breathing Apparatus and Associated Surveillance Records for January 2006 through
- HPCAL 2.15; Small Articles Monitor Type SAM 9/11 Calibration and Efficiency and Associated  
  December 2007
Calibration Record for Monitor No. 2; September 26, 2007  
-
- PC 75 Part 1; Monthly and Turnaround Maintenance for the Scott Model 4.5 Self-Contained  
                                                8                                Attachment
Breathing Apparatus and Associated Surveillance Records for January 2006 through  
December 2007  
-


- PBF-4077(c); Self-Contained Breathing Apparatus Inspection and Maintenance Records for
  2006 and 2007
9
- HPIP 4.51.4; Scott Self-Contained Breathing Apparatus; Revision 8
Attachment
Work Orders:
- PBF-4077(c); Self-Contained Breathing Apparatus Inspection and Maintenance Records for  
- CAP 01048997; Compliance with Fleet Procedure; September 8, 2006
2006 and 2007  
- CAP 01080787; Gamma-60 Source Check Concerns; March 6, 2007
- HPIP 4.51.4; Scott Self-Contained Breathing Apparatus; Revision 8  
- CAP 00906738; RP Survey Instrument Response Checks and Instrument Sign-Out;
Work Orders:  
  February 7, 2006
- CAP 01048997; Compliance with Fleet Procedure; September 8, 2006  
- CAP 01081898; Failure of Meter Movement for C-59 Area Monitor RE-111; March 13, 2007
- CAP 01080787; Gamma-60 Source Check Concerns; March 6, 2007  
- CAP 01091161; Lack of Bases for RP Equipment Functional Check; May 5, 2007
- CAP 00906738; RP Survey Instrument Response Checks and Instrument Sign-Out;  
- CAP 01087730; Possible Trend With Poor Teletector Performance; April 14, 2007
February 7, 2006  
4OA1 Performance Indicator Verification
- CAP 01081898; Failure of Meter Movement for C-59 Area Monitor RE-111; March 13, 2007  
Issue Reports:
- CAP 01091161; Lack of Bases for RP Equipment Functional Check; May 5, 2007  
- Monthly Data Elements for RETS/ODCM Radiological Effluents; December 2006 -
- CAP 01087730; Possible Trend With Poor Teletector Performance; April 14, 2007  
  November 2007
4OA1 Performance Indicator Verification
- Liquid and Gaseous Effluent Summary Data and Dose Calculation Results; March 2007
Issue Reports:  
4OA2 Problem Identification and Resolution
- Monthly Data Elements for RETS/ODCM Radiological Effluents; December 2006 -  
Procedures:
November 2007  
- NP 2.1.4 Operator Burdens; Revision 7
- Liquid and Gaseous Effluent Summary Data and Dose Calculation Results; March 2007
4OA3 Followup of Events and Notices of Enforcement Discretion
4OA2 Problem Identification and Resolution
Issue Reports:
Procedures:  
- CAP 01111841; RWST Temp Found High OOS on Logs; September 18, 2007
- NP 2.1.4 Operator Burdens; Revision 7  
- RCE 01111841-01; Unit 2 Refueling Water Storage Tank Temperature High Resulting in
4OA3 Followup of Events and Notices of Enforcement Discretion
  Unplanned TSAC; Revision 1
Issue Reports:  
- RCE 01090456-01; 1P-29 Turbine Driven Auxiliary Feedwater Pump Outboard Bearing Issues
- CAP 01111841; RWST Temp Found High OOS on Logs; September 18, 2007  
4OA5 Other Activities
- RCE 01111841-01; Unit 2 Refueling Water Storage Tank Temperature High Resulting in  
Documents:
Unplanned TSAC; Revision 1  
- EPRI Terry Turbine Guide; Terry Turbine Maintenance Guide, AFW Application TR-1007461
- RCE 01090456-01; 1P-29 Turbine Driven Auxiliary Feedwater Pump Outboard Bearing Issues  
- VTM 0004 Manual: Terry Steam Turbine Company; Auxiliary Feedwater Pump Turbine Drive;
4OA5 Other Activities  
  Revision 30
Documents:  
- Technical Data Sheet; Loctite High Temp Red
- EPRI Terry Turbine Guide; Terry Turbine Maintenance Guide, AFW Application TR-1007461  
- Technical Data Sheet; Turbo 50
- VTM 0004 Manual: Terry Steam Turbine Company; Auxiliary Feedwater Pump Turbine Drive;  
- Technical Data Sheet; Temp Tite II String Kit
Revision 30  
- RCE 01090456-01; IP-29 Turbine Driven Auxiliary Feedwater Pump Outboard Turbine Bearing
- Technical Data Sheet; Loctite High Temp Red  
  Issues
- Technical Data Sheet; Turbo 50
- MPR Report; Point Beach Nuclear Station; Water Containment of AFW Turbine Lube Oil
- Technical Data Sheet; Temp Tite II String Kit  
- Memo on OST Device Drain Plug - Justification of Drain Plug Removal
- RCE 01090456-01; IP-29 Turbine Driven Auxiliary Feedwater Pump Outboard Turbine Bearing  
- Station Logs - From Present Back to June 21, 2007; Focus on Auxiliary Feed Runs
Issues  
- OCC Logs - November 2006 Outage, September 2007 Overhaul, and November 2007
- MPR Report; Point Beach Nuclear Station; Water Containment of AFW Turbine Lube Oil  
  Overhaul
- Memo on OST Device Drain Plug - Justification of Drain Plug Removal  
- 2P-29 Event Folders
- Station Logs - From Present Back to June 21, 2007; Focus on Auxiliary Feed Runs  
- Applicable Oil Analysis Results Record
- OCC Logs - November 2006 Outage, September 2007 Overhaul, and November 2007  
                                                9                                Attachment
Overhaul  
- 2P-29 Event Folders  
- Applicable Oil Analysis Results Record  


- RCE 96-08; Unit 1 Reactor Taken Critical with Both 1P-29 Turbine-Driven Auxiliary Feedwater
  Pump Discharge Motor-Operated Valves (1AF-4000, 1AF-4001) Found Shut
10
- RCE 98-150; Unit 1 Turbine-Driven Auxiliary Feed Pump Turbine Maintenance Rework
Attachment
- RCE 01115748; 2P-29 AFW Pump Moisture in Oil
- RCE 96-08; Unit 1 Reactor Taken Critical with Both 1P-29 Turbine-Driven Auxiliary Feedwater  
Procedures:
Pump Discharge Motor-Operated Valves (1AF-4000, 1AF-4001) Found Shut  
- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul
- RCE 98-150; Unit 1 Turbine-Driven Auxiliary Feed Pump Turbine Maintenance Rework  
- IT-09A; Cold Start of Turbine-Driven Auxiliary Feed Pump and Valve Test
- RCE 01115748; 2P-29 AFW Pump Moisture in Oil  
- OI-62B; Turbine-Driven Auxiliary Feedwater System
Procedures:  
Condition Reports and Work Orders:
- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul  
- CAP 01049806; 1P-29 AFW Pump S/D Due to Low Oil Level in Bubbler; September 12, 2006
- IT-09A; Cold Start of Turbine-Driven Auxiliary Feed Pump and Valve Test  
- CAP 01051133; Oil Level Problems Encountered During PMT for 1P-29 AFP;
- OI-62B; Turbine-Driven Auxiliary Feedwater System  
  September 19, 2006
Condition Reports and Work Orders:  
- CAP 01062958; Reinstallation of Insulation for 2P-29 TDAFW Pump not Done;
- CAP 01049806; 1P-29 AFW Pump S/D Due to Low Oil Level in Bubbler; September 12, 2006  
  November 20, 2006
- CAP 01051133; Oil Level Problems Encountered During PMT for 1P-29 AFP;  
- CAP 01068606; 1P-29 Aux Feed Pump Suction Sodium Lab Analysis was High;
September 19, 2006  
  December 20, 2006
- CAP 01062958; Reinstallation of Insulation for 2P-29 TDAFW Pump not Done;  
- CAP 01086108; Additional Paint Removal Required - Not correctly Identified; April 5, 2007
November 20, 2006  
- CAP 01097185; Differences Noted Between RMP 9044-1 and EPRI Guide; June 17, 2007
- CAP 01068606; 1P-29 Aux Feed Pump Suction Sodium Lab Analysis was High;  
- CAP 01097732; Improvement Recommendations for RMP 9044-1; June 20, 2007
December 20, 2006  
- CAP 01097736; Declining Trend in 2P-29 TDAFW Pump Speed Noted; June 20, 2007
- CAP 01086108; Additional Paint Removal Required - Not correctly Identified; April 5, 2007  
- CAP 01098358; Moisture Observed in Oil Sample from 2P-29 Turbine Reservoir;
- CAP 01097185; Differences Noted Between RMP 9044-1 and EPRI Guide; June 17, 2007  
  June 21, 2007
- CAP 01097732; Improvement Recommendations for RMP 9044-1; June 20, 2007  
- CAP 01098364; AFW Steam Pipe Supports Lubra-Plates Have Been Painted; June 22, 2007
- CAP 01097736; Declining Trend in 2P-29 TDAFW Pump Speed Noted; June 20, 2007  
- CAP 01098445; Benchmark in Service Testing of Aux Feed Systems; June 22, 2007
- CAP 01098358; Moisture Observed in Oil Sample from 2P-29 Turbine Reservoir;  
- CAP 01098525; Unit 1 and 2 TDAFW Pump Oil Sampling; June 22, 2007
June 21, 2007  
- CAP 01098536; No Specific Training for Turbine Driven AFPs; June 22, 2007
- CAP 01098364; AFW Steam Pipe Supports Lubra-Plates Have Been Painted; June 22, 2007  
- CAP 01098615; U2R28 P-29-T: GL 89-13 HX PM Not Properly Documented; June 22, 2007
- CAP 01098445; Benchmark in Service Testing of Aux Feed Systems; June 22, 2007  
- CAP 01098626; AFW Casing Sealant Review; June 23, 2007
- CAP 01098525; Unit 1 and 2 TDAFW Pump Oil Sampling; June 22, 2007  
- CAP 01098633; 1P-29 TDAFW Pump Sentinel Valve Opened on Start; June 23, 2007
- CAP 01098536; No Specific Training for Turbine Driven AFPs; June 22, 2007  
- CAP 01099142; Unable to Analyze Water Content of Oil Sample; June 26, 2007
- CAP 01098615; U2R28 P-29-T: GL 89-13 HX PM Not Properly Documented; June 22, 2007  
- CAP 01099272; Oil Sample for 2P-29-T May Not Have Been Taken Correctly; June 26, 2007
- CAP 01098626; AFW Casing Sealant Review; June 23, 2007  
- CAP 01099402; 2007 AFW Inspection - Review of Additional Engineer Programs;
- CAP 01098633; 1P-29 TDAFW Pump Sentinel Valve Opened on Start; June 23, 2007  
  June 27, 2007
- CAP 01099142; Unable to Analyze Water Content of Oil Sample; June 26, 2007  
- CAP 01099576; 2P-29 TDAFWP Oil Sample High Water Content; June 28, 2007
- CAP 01099272; Oil Sample for 2P-29-T May Not Have Been Taken Correctly; June 26, 2007  
- CAP 01099876; Water Content Analysis Results for 2P-29-T OB Bearing; June 29, 2007
- CAP 01099402; 2007 AFW Inspection - Review of Additional Engineer Programs;  
- CAP 01100698; IT-08A/IT-09A Do Not Contain 1996 Reg Commitments; July 7, 2007
June 27, 2007  
- CAP 01100865; 1P-29-T Coupling Stretch Not Verified After Re-alignment; July 9, 2007
- CAP 01099576; 2P-29 TDAFWP Oil Sample High Water Content; June 28, 2007  
- CAP 01100874; RMP 9044-1 Contains Vague Guidance for Thomas Coupling Setting;
- CAP 01099876; Water Content Analysis Results for 2P-29-T OB Bearing; June 29, 2007  
  July 9, 2007
- CAP 01100698; IT-08A/IT-09A Do Not Contain 1996 Reg Commitments; July 7, 2007  
- CAP 01101114; Potential Preconditioning of 1(2)P-29 TDAFW Pump; July 11, 2007
- CAP 01100865; 1P-29-T Coupling Stretch Not Verified After Re-alignment; July 9, 2007  
- CAP 01101562; 2P-29 Oil Sample Put on HOLD by Supply Chain Buyer; July 12, 2007
- CAP 01100874; RMP 9044-1 Contains Vague Guidance for Thomas Coupling Setting;  
- CAP 01102282; 1P-29 Terry AFP Thomas Coupling Setting Concerns; July 18, 2007
July 9, 2007  
- CAP 01102417; RMP 9044-1, Revision 12, Provides Incorrect Acceptance Criteria;
- CAP 01101114; Potential Preconditioning of 1(2)P-29 TDAFW Pump; July 11, 2007  
  July 19, 2007
- CAP 01101562; 2P-29 Oil Sample Put on HOLD by Supply Chain Buyer; July 12, 2007  
- CAP 01102492; Quarantine Oil Samples Taken from 2P-29-T Under WO 335172;
- CAP 01102282; 1P-29 Terry AFP Thomas Coupling Setting Concerns; July 18, 2007  
  July 19, 2007
- CAP 01102417; RMP 9044-1, Revision 12, Provides Incorrect Acceptance Criteria;  
- CAP 01102642; 2P-029-T Oil Dripping from Outboard Bearing Housing Seal; July 19, 2007
July 19, 2007  
- CAP 01102655; Water Still Indicated in Oil from 2P-29-T OB BRG; July 20, 2007
- CAP 01102492; Quarantine Oil Samples Taken from 2P-29-T Under WO 335172;  
                                                10                                  Attachment
July 19, 2007  
- CAP 01102642; 2P-029-T Oil Dripping from Outboard Bearing Housing Seal; July 19, 2007  
- CAP 01102655; Water Still Indicated in Oil from 2P-29-T OB BRG; July 20, 2007  


- CAP 01102868; Higher Than Expected Water in 2P-29-T OB BRG Post Run Sample;
  July 21, 2007
11
- CAP 01102875; 2P-29 Appendix R Functionality; July 21, 2007
Attachment
- CAP 01102902; Documentation of Observation, 2P-29-T Temperature Indication;
- CAP 01102868; Higher Than Expected Water in 2P-29-T OB BRG Post Run Sample;  
  July 22, 2007
July 21, 2007  
- CAP 01102903; Verified Steam Leak at Seal on 2P-29-T OB Bearing; July 22, 2007
- CAP 01102875; 2P-29 Appendix R Functionality; July 21, 2007  
- CAP 01103469; Form for Bearing Stabilization on 1P-29 and 2P-29 Is Not Formalized;
- CAP 01102902; Documentation of Observation, 2P-29-T Temperature Indication;  
  July 25, 2007
July 22, 2007  
- CAP 01103520; Potential Improper Oil Issued for 2P-29 Aux Feed Pump; July 25, 2007
- CAP 01102903; Verified Steam Leak at Seal on 2P-29-T OB Bearing; July 22, 2007  
- CAP 01103623; Question Concerning Bearing Coolers on P-029 Turbines; July 26, 2007
- CAP 01103469; Form for Bearing Stabilization on 1P-29 and 2P-29 Is Not Formalized;  
- CAP 01103841; 1P-29T and 2P-29T OB Steam Gland Drain Lined Pitch Is Incorrect;
July 25, 2007  
  July 27, 2007
- CAP 01103520; Potential Improper Oil Issued for 2P-29 Aux Feed Pump; July 25, 2007  
- CAP 01106373; Evaluate Use of New Governor Drive Coupling on P-29T; August 10, 2007
- CAP 01103623; Question Concerning Bearing Coolers on P-029 Turbines; July 26, 2007  
- CAP 01107473; Oil Storage Requirements Questioned; August 17, 2007
- CAP 01103841; 1P-29T and 2P-29T OB Steam Gland Drain Lined Pitch Is Incorrect;  
- CAP 01108275; AFP Bearings Failed Vendor Dimensional Inspection; August 23, 2007
July 27, 2007  
- CAP 01108351; 2P-29-T Outboard Bearing Aluminum Fill Plug; August 23, 2007
- CAP 01106373; Evaluate Use of New Governor Drive Coupling on P-29T; August 10, 2007  
- CAP 01108355; 1P-29-T Oil Analysis Results Indicated As Alarm; August 23, 2007
- CAP 01107473; Oil Storage Requirements Questioned; August 17, 2007  
- CAP 01108426; 2P-29-T Governor Oil Level High; August 23, 2007
- CAP 01108275; AFP Bearings Failed Vendor Dimensional Inspection; August 23, 2007  
- CAP 01108429; Unexpected Oil Leak Rate While Running 2P-29-T; August 23, 2007
- CAP 01108351; 2P-29-T Outboard Bearing Aluminum Fill Plug; August 23, 2007  
- CAP 01108576; FPL AFW System Focused Assessment - Operations Observations;
- CAP 01108355; 1P-29-T Oil Analysis Results Indicated As Alarm; August 23, 2007  
  August 24, 2007
- CAP 01108426; 2P-29-T Governor Oil Level High; August 23, 2007  
- CAP 01109045; Oil Analysis Results Questioned; August 28, 2007
- CAP 01108429; Unexpected Oil Leak Rate While Running 2P-29-T; August 23, 2007  
- CAP 01109571; P-29-T Inbound Bearing Oiler Upper Casting Slightly Damaged;
- CAP 01108576; FPL AFW System Focused Assessment - Operations Observations;  
  August 31, 2007
August 24, 2007  
- CAP 01109572; 2P-29-T Oiler Height Settings; August 31, 2007
- CAP 01109045; Oil Analysis Results Questioned; August 28, 2007  
- CAP 01112474; 2P-29 Pump Outboard Packing Has Excessive Leakage; September 21, 2007
- CAP 01109571; P-29-T Inbound Bearing Oiler Upper Casting Slightly Damaged;  
- CAP 01112475; 2P-29 Outboard Turbine Bearing High Temp Alarm During IT-9A;
August 31, 2007  
  September 21, 2007
- CAP 01109572; 2P-29-T Oiler Height Settings; August 31, 2007  
- CAP 01112533; 2P-29-T Changing Oil and Stabilization; September 21, 2007
- CAP 01112474; 2P-29 Pump Outboard Packing Has Excessive Leakage; September 21, 2007  
- CAP 01112567; Terry Turbine Gland Case leak Off Lines Not Optimal; September 22, 2007
- CAP 01112475; 2P-29 Outboard Turbine Bearing High Temp Alarm During IT-9A;  
- CAP 01112579; Wrong Revision of Procedure Used for 2P-29-T Work; September 22, 2007
September 21, 2007  
- CAP 01112587; 2P-29-T TDAF Wheel Lap Measurement; September 22, 2007
- CAP 01112533; 2P-29-T Changing Oil and Stabilization; September 21, 2007  
- CAP 01112596; September 21, 2007 2P-29 Oil Analysis Results; September 22, 2007
- CAP 01112567; Terry Turbine Gland Case leak Off Lines Not Optimal; September 22, 2007  
- CAP 01112597; 2P-29-T Outboard Terry Turbine Bearing; September 22, 2007
- CAP 01112579; Wrong Revision of Procedure Used for 2P-29-T Work; September 22, 2007  
- CAP 01112609; 2P-29-T Outboard BRG Thermocouple Damaged During BRG Crush;
- CAP 01112587; 2P-29-T TDAF Wheel Lap Measurement; September 22, 2007  
  September 23, 2007
- CAP 01112596; September 21, 2007 2P-29 Oil Analysis Results; September 22, 2007  
- CAP 01112626; 2P-29-T Outboard Bearing Oil Ring Contacting Oil Cooler;
- CAP 01112597; 2P-29-T Outboard Terry Turbine Bearing; September 22, 2007  
  September 23, 2007
- CAP 01112609; 2P-29-T Outboard BRG Thermocouple Damaged During BRG Crush;  
- CAP 01112631; 2P-29-T Terry Turbine Casing Bolts; September 23, 2007
September 23, 2007  
- CAP 01112641; RMP 9044-1 Did Not Have Correct torque Value; September 23, 2007
- CAP 01112626; 2P-29-T Outboard Bearing Oil Ring Contacting Oil Cooler;
- CAP 01112660; 2P-29-T OB BRG Water Following IT-09A; September 24, 2007
September 23, 2007  
- CAP 01113029; RMP 9044-1 Wrong Revision Used for 2P-29-T Work; September 25, 2007
- CAP 01112631; 2P-29-T Terry Turbine Casing Bolts; September 23, 2007  
- CAP 01113318; IT-09A Oil Analysis Results Not As Expected for 2P-29-T;
- CAP 01112641; RMP 9044-1 Did Not Have Correct torque Value; September 23, 2007  
  September 27, 2007
- CAP 01112660; 2P-29-T OB BRG Water Following IT-09A; September 24, 2007  
- CAP 01113438; P-29-T Oil Cooler Differences Outboard End; October 1, 2007
- CAP 01113029; RMP 9044-1 Wrong Revision Used for 2P-29-T Work; September 25, 2007  
- CAP 01113972; IT-290B and IT-295B Makes Reference to Replaced ERPI Guide;
- CAP 01113318; IT-09A Oil Analysis Results Not As Expected for 2P-29-T;  
  October 10, 2007
September 27, 2007  
- CAP 01113973; Differences Between EPRI Guide and IT-08A, B and IT-09A,B;
- CAP 01113438; P-29-T Oil Cooler Differences Outboard End; October 1, 2007  
  October 10, 2007
- CAP 01113972; IT-290B and IT-295B Makes Reference to Replaced ERPI Guide;  
- CAP 01113978; EPRI Terry Turbine Manual Recommendation for AF; October 10, 2007
October 10, 2007  
- CAP 01115697; 2P-29 TDAFP Inbound Pump Bearing Oil Leak; November 1, 2007
- CAP 01113973; Differences Between EPRI Guide and IT-08A, B and IT-09A,B;  
                                            11                                  Attachment
October 10, 2007  
- CAP 01113978; EPRI Terry Turbine Manual Recommendation for AF; October 10, 2007  
- CAP 01115697; 2P-29 TDAFP Inbound Pump Bearing Oil Leak; November 1, 2007  


- CAP 01115748; 2P-29 Moisture in Oil Concern; November 1, 2007
- CAP 01115768; Visual Indications Post IR-09A on November 2, 2007 for Oil;
12
  November 2, 2007
Attachment
- CAP 01115778; Oil Sampling Concerns for 2P-29 AFW Pump; November 2, 2007
- CAP 01115748; 2P-29 Moisture in Oil Concern; November 1, 2007  
- CAP 01115808; Oil Analysis Results for 2P-29-T on November 3, 2007; November 3, 2007
- CAP 01115768; Visual Indications Post IR-09A on November 2, 2007 for Oil;  
- CAP 01115810; 2P-29 Returned to OPS in an Operable But Degraded Condition;
November 2, 2007  
  November 3, 2007
- CAP 01115778; Oil Sampling Concerns for 2P-29 AFW Pump; November 2, 2007  
- CAP 01115819; November 2, 2007 Log Entry for 2P-29 Availability Incomplete;
- CAP 01115808; Oil Analysis Results for 2P-29-T on November 3, 2007; November 3, 2007  
  November 4, 2007
- CAP 01115810; 2P-29 Returned to OPS in an Operable But Degraded Condition;  
- CAP 01115832; Appears Samples Not Taken Per Request; November 5, 2007
November 3, 2007  
- CAP 01115952; Oil Analysis Results for 2P-29-T from November 5, 2007; November 6, 2007
- CAP 01115819; November 2, 2007 Log Entry for 2P-29 Availability Incomplete;  
- CAP 01116158; 2P-29 Governor Gear Drive Oil Color; November 8, 2007
November 4, 2007  
- WO 219237; Uncouple 2P-29 Per Callup Text; March 8, 2006
- CAP 01115832; Appears Samples Not Taken Per Request; November 5, 2007  
- WO 219238; Inspect Inboard and Outboard Bearing; March 8, 2006
- CAP 01115952; Oil Analysis Results for 2P-29-T from November 5, 2007; November 6, 2007  
- WO 219239; Emergency Governor Inspection; March 8, 2006
- CAP 01116158; 2P-29 Governor Gear Drive Oil Color; November 8, 2007  
- WO 219240; Sample Oil in 2P-29 Turbine Governor; March 8, 2006
- WO 219237; Uncouple 2P-29 Per Callup Text; March 8, 2006  
- WO 219448; Perform Overhaul; October 24, 2006
- WO 219238; Inspect Inboard and Outboard Bearing; March 8, 2006  
- WO 267802; ten-Year Overhaul; November 12, 2006
- WO 219239; Emergency Governor Inspection; March 8, 2006  
- WO 268232; Sample Oil in 2P-29 Turbine Governor; November 12, 2006
- WO 219240; Sample Oil in 2P-29 Turbine Governor; March 8, 2006  
- WO 268233; GL 89-13 - Inspect Bearing Oil Coolers; November 12, 2006
- WO 219448; Perform Overhaul; October 24, 2006  
- WO 268234; Emergency Governor Inspection; November 12, 2006
- WO 267802; ten-Year Overhaul; November 12, 2006  
- WO 268235; Uncouple 2P-29 Pump from Its Turbine; November 12, 2006
- WO 268232; Sample Oil in 2P-29 Turbine Governor; November 12, 2006  
- WO 334308 Auxiliary Feedwater Pump Terry Turbine Overhaul; September 12, 2007
- WO 268233; GL 89-13 - Inspect Bearing Oil Coolers; November 12, 2006  
- WO 334597; Sample and Change Oil as Required; November 9, 2007
- WO 268234; Emergency Governor Inspection; November 12, 2006  
- WO 335167; Sample and Change Oil As Required; June 28, 2007
- WO 268235; Uncouple 2P-29 Pump from Its Turbine; November 12, 2006  
- WO 346758; Auxiliary Feedwater Pump Terry Turbine Overhaul; November 2, 2007
- WO 334308 Auxiliary Feedwater Pump Terry Turbine Overhaul; September 12, 2007  
NRC-Identified Condition Reports
- WO 334597; Sample and Change Oil as Required; November 9, 2007  
- AR 01100068; Closeout Based on Incorrect Info
- WO 335167; Sample and Change Oil As Required; June 28, 2007  
- AR 01100293; Benchmarking/Snapshot Evaluation for VTI
- WO 346758; Auxiliary Feedwater Pump Terry Turbine Overhaul; November 2, 2007  
- AR 01100509; Potential HU Crosscut
NRC-Identified Condition Reports
- AR 01100985; Cable ZA1327FA Not Included in App
- AR 01100068; Closeout Based on Incorrect Info  
- AR 01101029; Error Noted on Drawing WEST 499B466
- AR 01100293; Benchmarking/Snapshot Evaluation for VTI  
- AR 01101383; Near Miss During ILT NRC Exam
- AR 01100509; Potential HU Crosscut  
- AR 01101421; Untimely Corrective Actions
- AR 01100985; Cable ZA1327FA Not Included in App  
- AR 01101444; Compliance With Appendix R, Section III
- AR 01101029; Error Noted on Drawing WEST 499B466  
- AR 01101461; Potential Coincident Fire Induced Failure
- AR 01101383; Near Miss During ILT NRC Exam  
- AR 01101506; NFPA 13 Issues With G-01 and G-02 R
- AR 01101421; Untimely Corrective Actions  
- AR 01101596; Procedure EOP-3 Change Needed for Bistable Tube Rupture
- AR 01101444; Compliance With Appendix R, Section III  
- AR 01101667; Inconsistent/Inadequate Direction
- AR 01101461; Potential Coincident Fire Induced Failure  
- AR 01101704; Procedure EOP-3 Steps Out of Sequence
- AR 01101506; NFPA 13 Issues With G-01 and G-02 R  
- AR 01102113; Scaffold Clearance Questioned
- AR 01101596; Procedure EOP-3 Change Needed for Bistable Tube Rupture  
- AR 01102590; Incorrect Description of Pushbutton
- AR 01101667; Inconsistent/Inadequate Direction  
- AR 01103769; Error in Calculation S-11165-035-SW
- AR 01101704; Procedure EOP-3 Steps Out of Sequence  
- AR 01105181; Fire Extinguishers Removed for Annu
- AR 01102113; Scaffold Clearance Questioned  
- AR 01105290; Inappropriate Screened AR 11033415
- AR 01102590; Incorrect Description of Pushbutton  
- AR 01105804; PI Indicator Does Not Match INPO CD
- AR 01103769; Error in Calculation S-11165-035-SW  
- AR 01105948; PI-2849 Discharge Pressure on E SW
- AR 01105181; Fire Extinguishers Removed for Annu  
- AR 01105993; Quench Curve Check Performed
- AR 01105290; Inappropriate Screened AR 11033415  
- AR 01106042; Fluctuations Seen on P-32E SW Pump
- AR 01105804; PI Indicator Does Not Match INPO CD  
                                              12                              Attachment
- AR 01105948; PI-2849 Discharge Pressure on E SW  
- AR 01105993; Quench Curve Check Performed  
- AR 01106042; Fluctuations Seen on P-32E SW Pump  


- AR 01106118; Façade Groundwater Samples Not Shipped
- AR 01107098; Missing Bolts on Subsoil Drainage
13
- AR 01107355; Stalling of MOVs while Load Sequencing
Attachment
- AR 01107452; Lube oil Tank Rupture
- AR 01106118; Façade Groundwater Samples Not Shipped  
- AR 01107461; NRC RP Inspection: Groundwater
- AR 01107098; Missing Bolts on Subsoil Drainage  
- AR 01107485; Weakness Identified in 10 CFR 50.75(g)
- AR 01107355; Stalling of MOVs while Load Sequencing  
- AR 01107520; Debris in Subsoil Drainage System
- AR 01107452; Lube oil Tank Rupture  
- AR 01107630; Create Engineering Documents for Flooding
- AR 01107461; NRC RP Inspection: Groundwater  
- AR 01107634; Formally Verify Function and Capacity
- AR 01107485; Weakness Identified in 10 CFR 50.75(g)  
- AR 01108334; Radiodine Results High - Evaluate
- AR 01107520; Debris in Subsoil Drainage System  
- AR 01108724; Supplement Needed for LAR 249
- AR 01107630; Create Engineering Documents for Flooding  
- AR 01109665; LAR 247 submittal Being Withdrawn
- AR 01107634; Formally Verify Function and Capacity  
- AR 01109968; 2007 Mid-Cycle Performance Review
- AR 01108334; Radiodine Results High - Evaluate  
- AR 01109992; 2007 EP Drill
- AR 01108724; Supplement Needed for LAR 249  
- AR 01111043; LER 2007-003 Related AR Severity
- AR 01109665; LAR 247 submittal Being Withdrawn  
- AR 01111296; RCE-01075472 Not Revised per PARB
- AR 01109968; 2007 Mid-Cycle Performance Review  
- AR 01112896; Improvements in Posting and Access
- AR 01109992; 2007 EP Drill  
- AR 01112924; Postings in RCA Yard Found Faded
- AR 01111043; LER 2007-003 Related AR Severity  
- AR 01112934; Cleanliness in the Drumming Room
- AR 01111296; RCE-01075472 Not Revised per PARB  
- AR 01112981; Point Beach Nuclear Plant Flood Watch Commitment Information
- AR 01112896; Improvements in Posting and Access  
- AR 01113207; NRC Radwaste Inspection/ATCOR Equip
- AR 01112924; Postings in RCA Yard Found Faded  
- AR 01113226; NRC Question on 10 CFR 20, Appendix G, A.3
- AR 01112934; Cleanliness in the Drumming Room  
- AR 01113277; Material Condition
- AR 01112981; Point Beach Nuclear Plant Flood Watch Commitment Information  
- AR 01113347; NRC Radwaste Inspection Request
- AR 01113207; NRC Radwaste Inspection/ATCOR Equip  
- AR 01113420; NRC Inspection Debrief
- AR 01113226; NRC Question on 10 CFR 20, Appendix G, A.3  
- AR 01113508; Security Documentation Enhancement
- AR 01113277; Material Condition  
- AR 01113563; Security Weapons Documentation
- AR 01113347; NRC Radwaste Inspection Request  
- AR 01114426; Procedure Noncompliance of NP 8.4.1
- AR 01113420; NRC Inspection Debrief  
- AR 01114599; PC 99 May Need To Be Implemented
- AR 01113508; Security Documentation Enhancement  
- AR 01114637; Material in Yard
- AR 01113563; Security Weapons Documentation  
- AR 01114731; Loose Materials Found in the Protected Area
- AR 01114426; Procedure Noncompliance of NP 8.4.1  
- AR 01115102; Weakness Identified in Crew Information
- AR 01114599; PC 99 May Need To Be Implemented  
- AR 01115108; Unit 2 MFRV Turnover Less Than Complete
- AR 01114637; Material in Yard  
- AR 01115189; Scaffold Material in Contact
- AR 01114731; Loose Materials Found in the Protected Area  
- AR 01115311; Small Coolant Leak on G-04 EDG
- AR 01115102; Weakness Identified in Crew Information  
- AR 01115486; Point Beach Nuclear Plant Use of Maintenance Run
- AR 01115108; Unit 2 MFRV Turnover Less Than Complete  
- AR 01115556; Requirements of NP 7.7.5 for Maintenance
- AR 01115189; Scaffold Material in Contact
- AR 01115620; Error Found by Review of Maintenance
- AR 01115311; Small Coolant Leak on G-04 EDG  
- AR 01115703; OPR 01114308 Requires Revision
- AR 01115486; Point Beach Nuclear Plant Use of Maintenance Run
- AR 01115713; Number of Maintenance Rule Functional Failures
- AR 01115556; Requirements of NP 7.7.5 for Maintenance  
- AR 01115729; Documentation of D-06 Performance
- AR 01115620; Error Found by Review of Maintenance
- AR 01115818; Potential SSD Equipment Missing From Documentation
- AR 01115703; OPR 01114308 Requires Revision  
- AR 01115819; November 2, 2007 Log Entry for 2P-29
- AR 01115713; Number of Maintenance Rule Functional Failures  
- AR 01115820; LAR 256, ILRT Interval Extension
- AR 01115729; Documentation of D-06 Performance  
- AR 01115838; Revision 3 Required for OPR 1098358
- AR 01115818; Potential SSD Equipment Missing From Documentation  
- AR 01115876; EPRI Guidance Not Included in RMP 9
- AR 01115819; November 2, 2007 Log Entry for 2P-29  
- AR 01115881; Wording in OPR 1098358 May Be Misleading
- AR 01115820; LAR 256, ILRT Interval Extension  
- AR 01115951; Unit 2 TDAFWP Event - NRC Question
- AR 01115838; Revision 3 Required for OPR 1098358  
- AR 01115978; Watchstander Restriction Form Not Filed
- AR 01115876; EPRI Guidance Not Included in RMP 9  
- AR 01116011; 2P-29 Oil Samples
- AR 01115881; Wording in OPR 1098358 May Be Misleading  
- AR 01116150; Discrepancy in TAN Values
- AR 01115951; Unit 2 TDAFWP Event - NRC Question  
                                            13                            Attachment
- AR 01115978; Watchstander Restriction Form Not Filed  
- AR 01116011; 2P-29 Oil Samples  
- AR 01116150; Discrepancy in TAN Values  


- AR 01116158; 2P-29 Governor Gear Drive Oil Color
- AR 01116250; Lack of Sample Splitting Procedure
14
- AR 01116334; Minor Shaft Pitting - 2P-29
Attachment
- AR 01116442; 2P-029-T Oil Dregs
- AR 01116158; 2P-29 Governor Gear Drive Oil Color  
- AR 01116533; LAR 256 ILRT Extension Request
- AR 01116250; Lack of Sample Splitting Procedure  
- AR 01116589; MSPI Records Missing From EDMS
- AR 01116334; Minor Shaft Pitting - 2P-29  
- AR 01116594; HPIT - Confirmation Bias in Engineering
- AR 01116442; 2P-029-T Oil Dregs  
- AR 01116619; 2P-29-T - OPR Testing Methodology
- AR 01116533; LAR 256 ILRT Extension Request  
- AR 01116647; Procedural Temporary Change Chart
- AR 01116589; MSPI Records Missing From EDMS  
- AR 01116658; General Observations Regarding 2P-0
- AR 01116594; HPIT - Confirmation Bias in Engineering  
- AR 01116673; Clarification Needed for Sealant
- AR 01116619; 2P-29-T - OPR Testing Methodology  
- AR 01116688; Review/Revise OPR 1098358
- AR 01116647; Procedural Temporary Change Chart  
- AR 01116794; Minor Error Found in CDE
- AR 01116658; General Observations Regarding 2P-0  
- AR 01116819; Unavailability Guidance for MR and NEI
- AR 01116673; Clarification Needed for Sealant  
- AR 01117062; 1RMP-9096 and SLP 2 Revisions Required
- AR 01116688; Review/Revise OPR 1098358  
- AR 01117126; Revise/Correct EOP Setpoint for L.25 and L.4
- AR 01116794; Minor Error Found in CDE  
- AR 01117152; Revise IP-29 Root Cause to Address Issue
- AR 01116819; Unavailability Guidance for MR and NEI  
- AR 01117163; MI 32.9 Scaffold Stabilization Criteria
- AR 01117062; 1RMP-9096 and SLP 2 Revisions Required  
- AR 01117170; Rubber Pads Not Installed on RCP
- AR 01117126; Revise/Correct EOP Setpoint for L.25 and L.4  
- AR 01117200; NRC Noted Service Water Drawing - Verification Temperature Indicator
- AR 01117152; Revise IP-29 Root Cause to Address Issue  
- AR 01117205; NRC Noted Auxiliary Feedwater Drawing
- AR 01117163; MI 32.9 Scaffold Stabilization Criteria  
- AR 01117350; IT 40/45 Do Not Contain Caution Statements
- AR 01117170; Rubber Pads Not Installed on RCP  
- AR 01117459; Façade Wells - H-3 in Ground Water
- AR 01117200; NRC Noted Service Water Drawing - Verification Temperature Indicator  
- AR 01117637; Errors in Calculations - PCI-5344-S02
- AR 01117205; NRC Noted Auxiliary Feedwater Drawing  
- AR 01117860; Provide Preliminary Technical Basis - Temporary Storage Items
- AR 01117350; IT 40/45 Do Not Contain Caution Statements  
- AR 01118002; Errors in Calculations - PCI-5344-S01
- AR 01117459; Façade Wells - H-3 in Ground Water  
- AR 01118105; ACE 10434692 - Actions Not Identified
- AR 01117637; Errors in Calculations - PCI-5344-S02  
- AR 01118106; PM-7 Functional Check Periodicity
- AR 01117860; Provide Preliminary Technical Basis - Temporary Storage Items  
- AR 01118107; H3 Sample Results
- AR 01118002; Errors in Calculations - PCI-5344-S01  
- AR 01118141; License Amendment Quality/Timeliness
- AR 01118105; ACE 10434692 - Actions Not Identified  
- AR 01118144; Errors in Structural Calculation
- AR 01118106; PM-7 Functional Check Periodicity  
- AR 01118148; Rigging Evaluation Documentation
- AR 01118107; H3 Sample Results  
- AR 01118185; Evaluate Load Handling Procedure
- AR 01118141; License Amendment Quality/Timeliness  
- AR 01118189; NRC BL 2007-01, Security Officer
- AR 01118144; Errors in Structural Calculation  
- AR 01118194; Recommended Improvement to DG-M10
- AR 01118148; Rigging Evaluation Documentation  
- AR 01118195; SCBA LP Does Not Show How to Change
- AR 01118185; Evaluate Load Handling Procedure  
- AR 01118200; Support Model in Calculation PBNP-9
- AR 01118189; NRC BL 2007-01, Security Officer  
- AR 01118202; Low Design Margin for Plant Component
- AR 01118194; Recommended Improvement to DG-M10  
- AR 01118207; SCBA Monthly Location Inspection
- AR 01118195; SCBA LP Does Not Show How to Change  
- AR 01118213; Consider Completing and Audit on SC
- AR 01118200; Support Model in Calculation PBNP-9  
- AR 01118259; NRC Inspection Observation
- AR 01118202; Low Design Margin for Plant Component  
- AR 01118722; NRC Concern About Secondary Sample
- AR 01118207; SCBA Monthly Location Inspection  
- AR 01118844; Clarification Regarding Operability - Implement Recommendations
- AR 01118213; Consider Completing and Audit on SC  
- AR 01118847; NRC Submittal Rejected
- AR 01118259; NRC Inspection Observation  
                                              14                              Attachment
- AR 01118722; NRC Concern About Secondary Sample  
- AR 01118844; Clarification Regarding Operability - Implement Recommendations  
- AR 01118847; NRC Submittal Rejected  


                          LIST OF ACRONYMS USED
AC   Alternating Current
15
ACE   Apparent Cause Evaluation
Attachment
AFW   Auxiliary Feedwater
LIST OF ACRONYMS USED  
AOP   Abnormal Operating Procedure
AC  
ARM   Area Radiation Monitor
Alternating Current  
ASME American Society of Mechanical Engineers
ACE  
CAP   Corrective Action Program Document (Condition Report)
Apparent Cause Evaluation  
CEDE Committed Effective Dose Equivalent
AFW  
CFR   Code of Federal Regulations
Auxiliary Feedwater
CoC   Certificate of Compliance
AOP  
DRP   Division of Reactor Projects
Abnormal Operating Procedure  
DRS   Division of Reactor Safety
ARM  
EDG   Emergency Diesel Generator
Area Radiation Monitor  
EOP   Emergency Operating Procedure
ASME  
EPRI Electric Power Research Institute
American Society of Mechanical Engineers  
FSAR Final Safety Analysis Report
CAP  
IEEE Institute of Electrical & Electronic Engineers
Corrective Action Program Document (Condition Report)  
IMC   Inspection Manual Chapter
CEDE  
IP   Inspection Procedure
Committed Effective Dose Equivalent  
ips   Inches Per Second
CFR  
IR   Inspection Report
Code of Federal Regulations  
ISI   Inservice Inspection
CoC  
IST   Inservice Test
Certificate of Compliance  
IV   Independent Verification
DRP  
JPM   Job Performance Measure
Division of Reactor Projects  
kV   Kilovolt
DRS  
kW   Kilowatt
Division of Reactor Safety  
LCO   Limiting Condition for Operation
EDG  
LER   Licensee Event Report
Emergency Diesel Generator  
LHRA Locked High Radiation Area
EOP  
LOCA Loss of Coolant Accident
Emergency Operating Procedure  
LOOP Loss of Off-site Power
EPRI  
LORT Licensed Operator Requalification Training
Electric Power Research Institute  
MG   Motor-Generator
FSAR  
MOV   Motor-Operated Valve
Final Safety Analysis Report  
mrem Millirem
IEEE  
MSPI Mitigating Systems Performance Index
Institute of Electrical & Electronic Engineers  
NCV   Non-Cited Violation
IMC  
NEI   Nuclear Energy Institute
Inspection Manual Chapter  
NIOSH National Institute of Safety & Health
IP  
NMC   Nuclear Management Corporation
Inspection Procedure  
NRC   U.S. Nuclear Regulatory Commission
ips  
ODCM Offsite Dose Calculation Manual
Inches Per Second  
OM   Operational Maintenance
IR  
OPR   Operability Evaluation
Inspection Report  
OWA   Operator Workaround
ISI  
PI   Performance Indicator
Inservice Inspection  
PI&R Problem Identification and Resolution
IST  
PM   Planned or Preventative Maintenance
Inservice Test  
                                        15                Attachment
IV  
Independent Verification  
JPM  
Job Performance Measure  
kV  
Kilovolt
kW  
Kilowatt  
LCO  
Limiting Condition for Operation  
LER  
Licensee Event Report  
LHRA  
Locked High Radiation Area  
LOCA  
Loss of Coolant Accident  
LOOP  
Loss of Off-site Power  
LORT  
Licensed Operator Requalification Training  
MG  
Motor-Generator  
MOV  
Motor-Operated Valve  
mrem  
Millirem  
MSPI  
Mitigating Systems Performance Index  
NCV  
Non-Cited Violation  
NEI  
Nuclear Energy Institute  
NIOSH  
National Institute of Safety & Health  
NMC  
Nuclear Management Corporation  
NRC  
U.S. Nuclear Regulatory Commission  
ODCM  
Offsite Dose Calculation Manual  
OM  
Operational Maintenance  
OPR  
Operability Evaluation  
OWA  
Operator Workaround  
PI  
Performance Indicator  
PI&R  
Problem Identification and Resolution  
PM  
Planned or Preventative Maintenance  


PMT   Post-Maintenance Testing
ppm   Parts Per Million
16
PRA   Probabilistic Risk Assessment
Attachment
QA   Quality Assurance
PMT  
RCA   Radiologically Controlled Area
Post-Maintenance Testing  
RCE   Root Cause Evaluation
ppm  
RETS Radiological Effluent Technical Specification
Parts Per Million  
RHR   Residual Heat Removal
PRA  
RP   Radiation Protection
Probabilistic Risk Assessment  
RPS   Reactor Protection System
QA  
RPV   Reactor Pressure Vessel
Quality Assurance  
RWST Refueling Water Storage Tank
RCA  
SAT   Systems Approach to Training
Radiologically Controlled Area  
SCBA Self-Contained Breathing Apparatus
RCE  
SDP   Significance Determination Process
Root Cause Evaluation  
SSC   Structure, System, or Component
RETS  
SW   Service Water
Radiological Effluent Technical Specification  
TDAFW Turbine-Driven Auxiliary Feedwater
RHR  
TS   Technical Specification
Residual Heat Removal  
URI   Unresolved Item
RP  
WO   Work Order
Radiation Protection  
VIO   Violation
RPS  
                                      16            Attachment
Reactor Protection System  
RPV  
Reactor Pressure Vessel  
RWST  
Refueling Water Storage Tank  
SAT  
Systems Approach to Training  
SCBA  
Self-Contained Breathing Apparatus  
SDP  
Significance Determination Process  
SSC  
Structure, System, or Component  
SW  
Service Water  
TDAFW  
Turbine-Driven Auxiliary Feedwater  
TS  
Technical Specification  
URI  
Unresolved Item  
WO  
Work Order  
VIO  
Violation
}}
}}

Latest revision as of 18:05, 14 January 2025

IR 05000266-07-005, 05000301-07-005 on 10/01/2007 - 12/31/2007 for Point Beach, Units 1 & 2, Adverse Weather Protection, Operability Evaluations, Followup of Events, Other Activities
ML080450234
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 02/13/2008
From: Michael Kunowski
NRC/RGN-III/DRP/B5
To: Mccarthy J
Florida Power & Light Energy Point Beach
References
FOIA/PA-2010-0209 IR-07-005
Download: ML080450234 (69)


See also: IR 05000266/2007005

Text

February 13, 2008

Mr. James McCarthy

Site Vice President

FPL Energy Point Beach, LLC

6610 Nuclear Road

Two Rivers, WI 54241

SUBJECT:

POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED

INSPECTION REPORT 05000266/2007005 AND 05000301/2007005

Dear Mr. McCarthy:

On December 31, 2007, the U.S. Nuclear Regulatory Commission (NRC)

completed an integrated inspection at your Point Beach Nuclear Plant, Units 1 and 2.

The enclosed inspection report documents the inspection results, which were discussed

on January 10, 2008, with you and members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations, and with the conditions of your

license. The inspectors reviewed selected procedures and records, observed activities, and

interviewed your personnel.

Based on the results of this inspection, seven NRC-identified and self-revealed findings of very

low safety significance (Green) were identified. Five of these findings were determined to

involve violations of NRC requirements. However, because of the very low safety significance

and because they are entered into your corrective action program, the NRC is treating these

findings as Non-Cited Violations (NCVs), consistent with Section VI.A.1 of the NRC

Enforcement Policy. If you contest any NCV in this report, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC

20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the Resident Inspector Office at the Point Beach Nuclear Plant.

J. McCarthy

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in

the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Michael A. Kunowski, Chief

Branch 5

Division of Reactor Projects

Docket Nos. 50-266; 50-301

License Nos. DPR-24; DPR-27

Enclosure:

Inspection Report 05000266/2007005; 05000301/2007005

w/Attachment: Supplemental Information

cc w/encl:

M. Nazar, Senior Vice President and Nuclear

Chief Operating Officer

J. Stall, Senior Vice President and

Chief Nuclear Officer

R. Kundalkar, Vice President, Nuclear Technical Services

Licensing Manager, Point Beach Nuclear Plant

M. Ross, Managing Attorney

A. Fernandez, Senior Attorney

K. Duveneck, Town Chairman

Town of Two Creeks

Chairperson

Public Service Commission of Wisconsin

J. Kitsembel, Electric Division

Public Service Commission of Wisconsin

State Liaison Officer

J. McCarthy

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in

the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

Michael A. Kunowski, Chief

Branch 5

Division of Reactor Projects

Docket Nos. 50-266; 50-301

License Nos. DPR-24; DPR-27

Enclosure:

Inspection Report 05000266/2007005; 05000301/2007005

w/Attachment: Supplemental Information

cc w/encl:

M. Nazar, Senior Vice President and Nuclear

Chief Operating Officer

J. Stall, Senior Vice President and

Chief Nuclear Officer

R. Kundalkar, Vice President, Nuclear Technical Services

Licensing Manager, Point Beach Nuclear Plant

M. Ross, Managing Attorney

A. Fernandez, Senior Attorney

K. Duveneck, Town Chairman

Town of Two Creeks

Chairperson

Public Service Commission of Wisconsin

J. Kitsembel, Electric Division

Public Service Commission of Wisconsin

State Liaison Officer

DOCUMENT NAME: G:\\POIN\\Poin 2007 005.doc

Publicly Available

Non-Publicly Available

Sensitive

Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

NAME

RKrsek*MAK for

MKunowski

DATE

2/13/08

2/13/08

OFFICIAL RECORD COPY

Letter to J. McCarthy from M. Kunowski dated February 13, 2008.

SUBJECT:

POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED

INSPECTION REPORT 05000266/2007005 AND 05000301/2007005

DISTRIBUTION:

TEB

CFL

EMH1

LXR1

RidsNrrDirsIrib

MAS

KGO

JKH3

CAA1

RGK

LSL (electronic IRs only)

C. Pederson, DRP (hard copy - IRs only)

DRPIII

DRSIII

PLB1

TXN

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-266; 50-301

License Nos:

DPR-24; DPR-27

Report No:

05000266/2007005; 05000301/2007005

Licensee:

FPL Energy Point Beach, LLC

Facility:

Point Beach Nuclear Plant, Units 1 and 2

Location:

Two Rivers, Wisconsin

Dates:

October 1, 2007, through December 31, 2007

Inspectors:

R. Krsek, Senior Resident Inspector

R. Ruiz, Resident Inspector

S. Burton, Senior Resident Inspector, Kewaunee

P. Higgins, Resident Inspector, Kewaunee

W. Slawinski, Senior Health Physicist

C. Zoia, Operations Engineer

N. Valos, Senior Operations Engineer

K. Walton, Operations Engineer

R. Winter, Reactor Engineer

M. Jones, Reactor Engineer

Approved by:

Michael Kunowski, Chief

Branch 5

Division of Reactor Projects

2

Enclosure

SUMMARY OF FINDINGS

IR 05000266/2007005, 05000301/20070005; 10/01/2007-12/31/2007; Point Beach Nuclear

Plant, Units 1 & 2; Adverse Weather Protection; Operability Evaluations; Followup of Events;

Other Activities.

This report covers a three-month period of inspections by resident inspectors and regional

specialists. Seven Green findings were identified. Five of the findings which were identified

had associated Non-Cited Violations (NCVs). The significance of most findings is indicated

by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process, (SDP). Findings for which the SDP does not apply

may be Green or be assigned a severity level after NRC management review. The NRCs

program for overseeing the safe operation of commercial nuclear power reactors is described

in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors identified a finding of very low safety significance with no

associated violation of regulatory requirements for the licensees failure to control

loose materials in the protected area. Specifically, the inspectors identified

materials that were classified as tornado hazards per station procedure PC 99

near the Unit 1 and Unit 2 main and auxiliary transformers and the switchyard

boundary. Once notified, the licensee entered the issue into its corrective action

program and removed the materials. In addition, a procedure change request

was initiated to incorporate tornado hazard walkdowns into the abnormal

operating procedure for severe weather response.

The finding is more than minor because if left uncorrected, the loose items would

become a more significant safety concern. The finding is of very low safety

significance (Green) because it did not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment or functions will not be

available. Additionally, the inspectors determined that the finding had a cross-

cutting aspect in the area of problem identification and resolution in that the

licensee failed to take appropriate corrective actions to address safety issues and

adverse trends in a timely manner, commensurate with their safety significance

and complexity (P.1(d)). (Section 1R01.1)

Cornerstone: Mitigating Systems

Green. A self-revealed finding with no associated violation of regulatory

requirements was identified for an inadequate operability evaluation performed

in June 2007 for service water pump P-32C. Specifically, the pump failed its

inservice test (IST) on high vibrations after approximately six hours of operation,

but the operability evaluation had concluded the pump vibrations would not reach

the out-of-service limit until after 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> of continuous operation. Contributing

to the unanticipated early failure was the use of non-conservative decision-

making and the use of a non-conservative assumption in the pumps vibration

prediction model. The licensee entered this issue into its corrective action

program and P-32C was subsequently repaired and returned to service.

3

Enclosure

The finding is more than minor because it could reasonably be viewed as a

precursor to a significant event. The finding is of very low safety significance

(Green) because there was no design deficiency, no actual loss of safety

function, no single train loss of safety function for greater than the Technical

Specification (TS) allowed outage time, and no risk due to external events.

Additionally, the inspectors determined that the finding had a cross-cutting aspect

in the area of human performance. Specifically, the licensee failed to use

conservative assumptions in decision-making affecting operability of safety-

related equipment (H.1(b)). (Section 1R15.1)

Green. The inspectors identified a finding of very low safety significance (Green)

and an associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, for the failure to adequately assess

operability of the Unit 2 2P-29 turbine-driven auxiliary feedwater (TDAFW) pump.

The licensee failed to implement procedural requirements regarding the

immediate assessment of operability on September 24 and September 27, 2007,

for the increased water ingress into the turbine outboard bearing housing for the

pump following maintenance activities. The licensee took corrective actions,

which included performing an operability evaluation on November 1 when the

next scheduled test again revealed higher than normal levels of water in the

bearing oil. However, the inspectors continued to identify, in the subsequent

revisions to the operability determination, that the licensee failed to utilize all the

data available to assess pump operability. At the end of the inspection period,

the licensee continued to evaluate the causes and corrective actions to address

this finding.

The finding is more than minor because, if left uncorrected, the failure to properly

assess operability would result in the TDAFW pump being degraded, and

possibly inoperable for more than the allowed outage time in accordance with

TSs with no action being taken. The finding is of very low safety significance

(Green) because the inadequate operability determination did not result in

exceeding the allowed outage time of TSs before action was taken. Additionally,

the inspectors determined that the finding had a cross-cutting aspect in the area

of human performance. Specifically, the licensee failed to use conservative

assumptions in decision-making affecting operability of safety-related equipment

(H.1(b)). (Section 1R15.2)

Green. A self-revealed finding and an associated Non-Cited Violation of

10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

were identified for the failure to have adequate procedures to allow operators to

properly set the thermostat of the Unit 2 refueling water storage tank (RWST)

heaters and to ensure the RWST was recirculated frequently enough for the

temperature indicator to accurately measure bulk temperature. On

September 18, 2007, the Unit 2 RWST was found to be at 105 °F. This

temperature exceeded the TS-maximum allowable limit of 100 °F (97 °F

parametric) and could not be restored to acceptable limits before the eight-hour

TS action statement expired. As a result, a shutdown of Unit 2 was commenced.

At 20 percent power, a return to full power began after the RWST temperature

was restored to within acceptable limits. It was later identified that the undesired

heat-up was caused by the incorrect setting of the controlling thermostat for the

RWST heaters.

4

Enclosure

The finding is more than minor because it is associated with the procedure

quality and human performance attributes of the Mitigating Systems Cornerstone

and affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage). The finding is of very low safety significance

(Green) because the elevated temperature of the RWST and subsequent

shutdown sequence did not contribute to both the likelihood of a reactor trip and

the likelihood that mitigation equipment or functions would not be available.

Additionally, the inspectors determined that the finding had a cross-cutting aspect

in the area of human performance. Specifically, human error prevention

techniques were not utilized prior to and during the thermostat setting task and

personnel proceeded in the face of uncertainty and unexpected circumstances

(H.4(a)). (Section 4OA3.1)

Green. The inspectors identified a finding of very low safety significance and an

associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, for the licensees failure to conduct

adequate post-maintenance testing of the Unit 1 1P-29 turbine-driven auxiliary

feedwater (TDAFW) pump following a ten-year overhaul of the turbine in

May 2007. Specifically, the ten-year overhaul maintenance included bearing

replacement, but the TDAFW pump was not run long enough during testing for

bearing temperature to stabilize. The appropriate post-maintenance test would

have detected that the bearing temperatures were rising and required evaluation

prior to declaring the TDAFW pump operable. The licensee entered the issue

into its corrective action program and took immediate corrective actions.

Additionally, the licensee initiated changes to the inadequate procedures.

The finding is more than minor because, if left uncorrected, the issue would have

become a more significant safety concern. The inspectors determined this

finding was not a design qualification deficiency resulting in a loss of function per

NRC Generic Letter 91-18, did not represent an actual loss of safety function of a

system or train of equipment, and was not potentially risk-significant due to a

seismic, fire, flooding, or severe weather initiating event. Therefore, the finding is

considered to be of very low safety significance (Green). Additionally, the

inspectors determined that the finding had a cross-cutting aspect in the area of

human performance. Specifically, the licensee failed to ensure that procedures

were adequate and accurate to assure nuclear safety (H.2(c)). (Section 4OA5.1)

Green. The inspectors identified a finding of very low safety significance and an

associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, for the failure to implement prompt corrective actions for the

degraded oil conditions initially identified with the Unit 2 2P-29 turbine-driven

auxiliary feedwater (TDAFW) pump on September 24, 2007, following

maintenance. Following an additional oil sample with favorable results, the

licensee incorrectly concluded, due to confirmational biases, that the high water

content of the first oil sample was an expected condition. The licensee wrote a

condition report, but it was closed with no actions taken. In November 2007, the

licensee identified that a significant degraded oil condition existed with the pump.

The licensee entered the issue into its corrective action program and took

immediate corrective actions, including rebuilding the pump turbine. The

5

Enclosure

licensee continued to evaluate the causes and corrective actions to address this

finding at the end of the inspection period.

The finding is more than minor because it could reasonably be viewed as a

precursor to a significant event. Specifically, the failure to correct the cause of

the oil degradation in a timely manner in September 2007 could have resulted in

the failure of the 2P-29 TDAFW pump. The finding is of very low safety

significance (Green) because there was no design deficiency, no actual loss of

safety function, no single train loss of safety function for greater than the TS

allowed outage time, and no risk due to external events. Additionally, the

inspectors determined that the finding had a cross-cutting area aspect in the

area of problem identification and resolution. Specifically, the licensee failed to

thoroughly evaluate the problem with water ingress into the oil, such that a

resolution addressed the cause and extent of condition (P.1(c)).

(Section 4OA5.2.b.1)

Cornerstone: Other

Green. The inspectors identified a finding of very low safety significance and

an associated Non-Cited Violation of 10 CFR 72.48(c)(1) for the licensees

failure to obtain a Certificate of Compliance (CoC) amendment pursuant to

10 CFR 72.244, for changes made in the spent fuel storage cask operating

procedures during the 2004 loading campaign as described in the Final Safety

Analysis Report. The procedure changes constituted a change in the terms,

conditions, or specifications incorporated in the CoC. Although the procedures

were contained in the Final Safety Analysis Report, the licensee failed to identify

that TS 1.2.17a, 32PT Dry Storage Canister (DSC) Vacuum Drying Duration

Limit, was also affected by the procedure change and required prior NRC

approval. The licensee implemented corrective actions, which included revising

the loading procedure to reflect the sequence described in the FSAR prior to the

next cask loading campaign.

This finding is more than minor because it had the potential to impact the NRCs

ability to perform its regulatory function, since the licensee failed to receive NRC

approval for a change in this licensed activity. The inspectors determined that

the finding was not suitable for SDP evaluation because the noncompliance

involved 10 CFR Part 72 dry fuel storage activities. Therefore, this finding was

reviewed by regional management and dispositioned using traditional

enforcement. The finding was determined to be of very low safety significance

(Green). (Section 4OA5.5)

B.

Licensee-Identified Violations

No violations of significance were identified.

6

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 was at 100 percent power throughout the inspection period with the exception of brief

reductions in power during routine auxiliary feedwater pump and secondary system valve

testing.

Unit 2 was at 100 percent power throughout the inspection period with the exception of brief

reductions in power during routine auxiliary feedwater pump and secondary system valve

testing.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1

Readiness For Impending Adverse Weather Condition - High Wind Conditions

a.

Inspection Scope

Because high winds were forecast in the vicinity of the facility for October 18, 2007, the

inspectors reviewed the licensees overall preparations for the expected weather

conditions. The inspectors walked down important outdoors areas within the protected

area, in addition to the licensees emergency alternating current (AC) power systems,

because safety-related functions could be affected by, or required as a result of, high

winds or tornado-generated missiles. The inspectors focused on the licensees

procedures used to respond to specified adverse weather conditions and toured the

plant grounds for loose debris, which could become missiles during a tornado or high

winds condition. The inspectors evaluated the licensees preparations against the sites

procedures and evaluated the adequacy of the staffs response. The inspectors also

verified that the licensee was identifying adverse weather issues at an appropriate

threshold and entering them into its corrective action program in accordance with station

procedures.

This inspection constituted one sample prior to the onset of an adverse weather.

b.

Findings

Introduction: The inspectors identified a finding of very low safety significance (Green)

for the licensees failure to control loose materials in the protected area. Specifically, the

inspectors identified materials that were classified as tornado hazards per licensee

procedure PC 99 and were near the Unit 1 and Unit 2 main and auxiliary transformers

and the switchyard boundary. No violation of regulatory requirements occurred.

Description: On October 18, 2007, the inspectors conducted a walkdown of the risk

significant portions of the main and auxiliary power system to assess the licensees

preparations to preclude or minimize potential damage from high winds associated with

severe storms or tornadoes. During the walkdown, the inspectors identified a significant

quantity of unsecured materials meeting the definition of tornado hazards provided in

7

Enclosure

Point Beach procedure PC 99, Tornado Hazards Inspection Checklist, near the subject

transformers. The inspectors concluded that high winds or tornadoes combined with the

proximity of the transformers to the large quantity of unsecured materials increased the

potential to damage the transformers or related electrical equipment. The inspectors

informed the licensee of the concern and the licensee took immediate corrective action

to clean the areas identified by the inspectors and entered the issue into the corrective

action program as corrective action program document (CAP, condition report)

CAP 01114731. The licensee also commenced a walkdown of outside areas within the

protected area to address extent of condition. In addition, the licensee initiated a

procedure change request to incorporate tornado hazard walkdowns into Abnormal

Operating Procedure (AOP) 13C, Severe Weather Conditions.

Analysis: The inspectors determined that the failure of licensee personnel to control

material in the protected area near risk significant equipment is a performance

deficiency. Using the guidance contained in Inspection Manual Chapter (IMC) 0612,

Power Reactor Inspection Reports. Appendix B, Issue Disposition Screening, dated

September 20, 2007, the inspectors determined that the finding is more than minor

because, if left uncorrected, the loose items in the vicinity of the main and auxiliary

transformers, and near the switchyard, would become a more significant safety concern.

The inspectors determined that the finding warranted evaluation using the Significance

Determination Process (SDP) because the finding is associated with an increase in the

likelihood of an initiating event.

The inspectors evaluated the finding using IMC 0609, Appendix A, Attachment 1,

Significance Determination of Reactor Inspection Findings for At-Power Situations,

dated January 10, 2008. Using the Phase 1 SDP worksheet for the Initiating Event

Cornerstone, transient initiator contributor, the inspectors determined that the finding did

not contribute to the likelihood of a primary or secondary system loss of coolant accident

initiator; the finding did not contribute to both the likelihood of a reactor trip and the

likelihood that mitigation equipment or functions will not be available; and the finding did

not increase the likelihood of a fire or internal or external flooding. Therefore, the finding

is determined to be of very low safety significance (Green).

The inspectors performed a review of past corrective action program documents to

assess the effectiveness of the licensees corrective actions to address similar issues.

During this review, inspectors noted that an NRC-identified finding, 05000266/000301-

2006004-01, was issued in July 2006 for a nearly identical issue related to the failure to

control loose material in the protected area. Procedure PC 99 was created as a

corrective action for that finding. In addition, inspectors noted that between May and

September 2007, there have been a number of CAPs written as a result of the

identification of tornado hazards in the protected area during the use of procedure

PC 99. Consequently, the inspectors determined that the finding had a cross-cutting

aspect in the area of problem identification and resolution. Specifically, the licensee

failed to take appropriate corrective actions to address safety issues and adverse trends

in a timely manner, commensurate with their safety significance and complexity (P.1(d)).

Enforcement: The failure to maintain the protected area free of tornado hazards was not

an activity affecting quality subject to 10 CFR Part 50, Appendix B, nor was a procedure

required by license conditions or TSs violated. Therefore, while a performance

deficiency existed, no violation of regulatory requirements occurred. This is considered

a finding of very low safety significance (FIN 05000266/2007005-01;

8

Enclosure 05000301/2007005-01). The licensee included this finding in its corrective action

program as CAP 01114731.

.2

Winter Seasonal Readiness Preparations

a.

Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant specific design features and the licensees procedures used

to prepare for the onset of cold weather. Additionally, the inspectors reviewed licensee

corrective actions for areas in the plant which previously had cold weather issues. Cold

weather protection equipment, such as the façade freeze heat tracing and temporary

area heaters, were verified to be in operation when applicable. The inspectors also

reviewed corrective action program items to verify that the licensee was identifying cold

weather issues at an appropriate threshold and entering them into the corrective action

program in accordance with procedures. The inspectors reviews focused specifically on

the following plant systems due to their risk significance or susceptibility to cold weather

issues: main steam system and instrumentation, including the atmospheric steam

dumps and the main steam isolation valve; emergency core cooling system, including

the refueling water storage tank and associated piping; and the façade freeze system.

This inspection constituted one winter seasonal system readiness sample.

b.

Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a.

Inspection Scope

The inspectors performed partial walkdowns of accessible portions of risk-significant

systems to determine the operability of these systems. The inspectors utilized system

valve lineup and electrical breaker checklists, tank level books, plant drawings, and

selected operating procedures to determine whether the systems were correctly aligned

to perform the intended design functions. The inspectors also examined the material

condition of the components and observed operating equipment parameters to

determine whether deficiencies existed. The inspectors reviewed completed work

orders (WOs) and calibration records associated with the systems for issues that could

affect component or train functions. The inspectors used the information in the

appropriate sections of the Final Safety Analysis Report (FSAR) to determine the

functional requirements of the system.

Partial system walkdowns of the following systems constituted two inspection procedure

samples:

9

Enclosure

Emergency diesel generator (EDG) G01 aligned to busses 1A05 and 2A05 while

EDG G02 was out-of-service the week of October 22, 2007; and

EDG G02 aligned to busses 1A05 and 2A05 while EDG G01 was out-of-service

the week of November 19, 2007.

b.

Findings

No findings of significance were identified.

.2

Semi-Annual Complete System Walkdown

a.

Inspection Scope

In November 2007, the inspectors performed a complete system alignment inspection of

the auxiliary feedwater (AFW) system for Units 1 and 2 to verify the functional capability

of the system. This system was selected because it was considered both safety-

significant and risk-significant in the licensees probabilistic risk assessment. The

inspectors walked down the system to review mechanical and electrical equipment line-

ups, electrical power availability, system pressure and temperature indications,

component labeling, component lubrication, component and equipment cooling, hangers

and supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. A review of past and outstanding WOs

was performed to determine whether any deficiencies significantly affected system

function. In addition, the inspectors reviewed the CAP database to ensure that system

equipment alignment problems were being identified and appropriately resolved. The

documents used for the walkdown and issue review are listed in the attached List of

Documents Reviewed.

These activities constituted one complete system walkdown inspection procedure

sample.

b.

Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection walkdowns, which focused on the following

attributes: the availability, accessibility, and condition of fire fighting equipment; the

control of transient combustibles and ignition sources; and the condition and status of

installed fire barriers. The inspectors selected fire areas for inspection based on the

areas overall fire risk contribution, as documented in the Individual Plant Examination of

External Events, or the potential of a fire to impact equipment that could initiate a plant

transient.

In addition, the inspectors assessed these additional fire protection attributes during

walkdowns: fire hoses and extinguishers were in the designated locations and available

10

Enclosure

for immediate use; unobstructed fire detectors and sprinklers; transient material loading

within the analyzed limits; and fire doors, dampers, and penetration seals in satisfactory

condition. The inspectors also determined whether minor issues identified during the

inspection were entered into the licensees corrective action program.

The walkdown of the following selected fire zones constituted three inspection procedure

samples:

Unit 2 TDAF Room

EDG G01 Room

EDG G02 Room

b.

Findings

No findings of significance were identified.

.2

Annual Fire Protection Drill Observation (71111.05A)

a.

Inspection Scope

During this quarter, the inspectors observed two fire brigade activation drills: an

October 9, 2007, drill scenario that simulated a fire in the Unit 2 2P-2C charging pump

room and a November 26 drill scenario that simulated a fire in the unit common cable

spreading room. The combined drill observations were used to determine the readiness

of the plant fire brigade to fight fires. The inspectors verified that the licensee staff

identified deficiencies, openly discussed them in a self-critical manner at the drill

debriefs, and took appropriate corrective actions. Specific attributes evaluated were:

(1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper

use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;

(4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade

leader communications, command, and control; (6) search for victims and propagation of

the fire into other plant areas; (7) smoke removal operations; (8) utilization of pre-

planned strategies; (9) adherence to the pre-planned drill scenario; and (10) drill

objectives.

These activities constituted one annual fire protection inspection sample.

b.

Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07)

a.

Inspection Scope

The inspectors reviewed the licensees testing of the EDG G01 and G02 heat

exchangers one month following their replacement to verify that potential deficiencies

did not affect the licensees ability to detect degraded performance, and to identify any

common cause issues that had the potential to increase risk, and to ensure that the

licensee was adequately addressing problems that could result in initiating events that

would cause an increase in risk. The inspectors also verified that the new heat

11

Enclosure

exchangers were less susceptible to lake grass fouling, than the original heat

exchangers. The inspectors reviewed the licensees observations as compared against

acceptance criteria, the correlation of scheduled testing and the frequency of testing,

and the impact of instrument inaccuracies on test results. Inspectors also verified that

test acceptance criteria considered differences between test conditions, design

conditions, and testing criteria.

This inspection constituted one inspection procedure sample.

b.

Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

.1

Resident Inspector Quarterly Review

a.

Inspection Scope

In November 2007, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator training to verify that operator performance was

adequate, evaluators were identifying and documenting crew performance problems,

and training was being conducted in accordance with licensee procedures. The

inspectors evaluated the following areas:

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements.

This inspection constituted one quarterly licensed operator requalification program

sample.

b.

Findings

No findings of significance were identified.

.2

Facility Operating History

a.

Inspection Scope

The inspectors reviewed the plants operating history from September 2005 through

October 2007 to identify operating experience that was expected to be addressed by the

12

Enclosure

Licensed Operator Requalification Training (LORT) program. It was then verified that

the identified operating experience had been addressed by the facility licensee in

accordance with the stations approved Systems Approach to Training (SAT) program to

satisfy the requirements of 10 CFR 55.59(c), Requalification program requirements.

b. Findings

No findings of significance were identified.

.3

Licensee Requalification Examinations

a.

Inspection Scope

The inspectors performed a biennial inspection of the licensees LORT test/examination

program for compliance with the stations SAT program that would satisfy the

requirements of 10 CFR 55.59(c)(4), Evaluation. The inspectors reviewed the 2006

biennial written requalification examinations and 2007 annual operating test material to

evaluate general quality, construction, and difficulty level. The written examinations

reviewed consisted of four written examinations, each containing 30 questions. The

operating examination material consisted of 6 operating tests, each containing

approximately two dynamic simulator scenarios and five job performance measures

(JPMs). The inspectors reviewed the annual requalification operating test and biennial

written examination material to evaluate general quality, construction, and difficulty level.

The inspectors assessed the level of examination material duplication from week-to-

week during the current year operating test and written examinations. The inspectors

reviewed the methodology for developing the examinations, including the LORT program

two-year sample plan, probabilistic risk assessment insights, previously identified

operator performance deficiencies, and plant modifications.

b.

Findings

No findings of significance were identified.

.4

Licensee Administration of Requalification Examinations

a.

Inspection Scope

The inspectors observed the administration of a requalification operating test to assess

the licensees effectiveness in conducting the test to ensure compliance with

10 CFR 55.59(c)(4), Evaluation. The inspectors evaluated the performance of one

crew in parallel with the facility evaluators during one dynamic simulator scenario and

evaluated various licensed crew members concurrently with facility evaluators during the

administration of several JPMs. The inspectors assessed the facility evaluators ability

to determine adequate crew and individual performance using objective, measurable

standards. The inspectors observed the training staff personnel administer the operating

test, including conducting pre-examination briefings, evaluations of operator

performance, and individual and crew evaluations upon completion of the operating test.

The inspectors evaluated the ability of the simulator to support the examinations. A

specific evaluation of simulator performance was conducted and documented under

Section 1R11.9 of this report.

13

Enclosure

b.

Findings

No findings of significance were identified.

.5

Examination Security

a.

Inspection Scope

The inspectors observed and reviewed the licensees overall licensed operator

requalification examination security program related to examination physical security

(e.g., access restrictions and simulator considerations) and integrity (e.g., predictability

and bias) to verify compliance with 10 CFR 55.49, Integrity of examinations and tests.

The inspectors also reviewed the facility licensees examination security procedure, any

corrective actions related to past or present examination security problems at the facility,

and the implementation of security and integrity measures (e.g., security agreements,

sampling criteria, bank use, and test item repetition) throughout the examination

process.

b.

Findings

There was one issue associated with examination security identified by the licensee

during the administration of JPMs during the sixth week of administration of the 2007

annual operating test. On October 31, 2007, an individual who had just completed a

simulator JPM was escorted back to the waiting room area and dropped off. However,

there was no examination sequesterer in the waiting room area to ensure that there was

no examination compromise with individuals in the room who had not been administered

the JPM. Within two minutes, the licensee identified the potential for an examination

compromise. The licensee determined that the individual who had just been

administered the JPM did not communicate any exam-related information to any other

individuals who had not been administered the JPM. As part of its corrective actions, the

licensee held a training department standdown with the members of the examination

team. The licensee replaced the JPM in question for the remaining individuals to be

tested. The issue was documented in the corrective action program as CAP 01115710.

The NRC was appropriately notified of the issue. The issue was reviewed and assessed

for a possible violation of 10 CFR 55.49, Integrity of examinations and tests. With the

actions taken, it was determined that no actual examination compromise had occurred.

The issue was not subject to enforcement action in accordance with NRC enforcement

policy.

.6

Licensee Training Feedback System

a.

Inspection Scope

The inspectors assessed the methods and effectiveness of the licensees processes

for revising and maintaining its LORT program up-to-date, including the use of feedback

from plant events and industry experience information. The inspectors reviewed the

licensees quality assurance oversight activities, including licensee training department

self-assessment reports. The inspectors evaluated the licensees ability to assess the

effectiveness of its LORT program and its ability to implement appropriate corrective

14

Enclosure

actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c)

Requalification program requirements, and the licensees SAT program.

b.

Findings

No findings of significance were identified.

.7

Licensee Remedial Training Program

a.

Inspection Scope

The inspectors assessed the adequacy and effectiveness of the remedial training

conducted since the previous biennial requalification examinations and the training from

the current examination cycle to ensure that they addressed weaknesses in licensed

operator or crew performance identified during training and plant operations. The

inspectors reviewed remedial training procedures and individual remedial training plans.

This evaluation was performed in accordance with 10 CFR 55.59(c), Requalification

program requirements, and with respect to the licensees SAT program.

b.

Findings

No findings of significance were identified.

.8

Conformance with Operator License Conditions

a. Inspection Scope

The inspectors reviewed the facility and individual operator licensees' conformance

with the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's

program for maintaining active operator licenses and to assess compliance with

10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the

process for tracking on-shift hours for licensed operators and which control room

positions were granted watch-standing credit for maintaining active operator licenses.

The inspectors reviewed the facility licensee's LORT program to assess compliance with

the requalification program requirements as described by 10 CFR 55.59(c). Additionally,

medical records for seven licensed operators were reviewed for compliance with

10 CFR 55.53(i).

b. Findings

No findings of significance were identified.

.9

Conformance with Simulator Requirements

a.

Inspection Scope

The inspectors assessed the adequacy of the licensees simulation facility (simulator) for

use in operator licensing examinations and for satisfying experience requirements as

prescribed in 10 CFR 55.46, Simulation facilities. The inspectors also reviewed a

sample of simulator performance test records (i.e., transient tests, malfunction tests, and

core performance tests), simulator discrepancies, and the process for ensuring

15

Enclosure

continued assurance of simulator fidelity in accordance with 10 CFR 55.46. The

inspectors reviewed and evaluated the discrepancy process to ensure that simulator

fidelity was maintained. Open simulator discrepancies were reviewed for importance

relative to the impact on 10 CFR 55.45 and 55.59 operator actions, as well as on nuclear

and thermal hydraulic operating characteristics. The inspectors interviewed the

licensees simulator staff about the configuration control process and completed the

Inspection Procedure 71111.11, Appendix C checklist, to evaluate whether the

licensees plant-referenced simulator was operating adequately as required by

10 CFR 55.46(c) and (d).

b.

Findings

No findings of significance were identified.

.10

Annual Operating Test Results

a.

Inspection Scope

The inspectors reviewed the overall pass/fail results of the annual JPM operating tests,

and the annual simulator operating tests (required to be given per 10 CFR 55.59(a)(2))

administered by the licensee during 2007. The overall results were compared with the

SDP in accordance with IMC 0609, Appendix I, Operator Requalification Human

Performance Significance Determination Process (SDP), dated August 22, 2005. The

year 2007 was the first year of the licensees 24-month training program; therefore, no

written examination was administered in 2007.

This represented one sample.

b.

Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed risk assessments for planned and emergent maintenance

activities during the specified work weeks. During these reviews, the inspectors

compared the licensees risk management actions to those actions specified in the

licensees procedures for the assessment and management of risk associated with

maintenance activities. The inspectors assessed whether evaluation, planning, control,

and performance of the work were done in a manner to reduce the risk and minimize the

duration, where practical, and whether contingency plans were in place where

appropriate.

The inspectors used the licensees daily configuration risk assessment records,

observations of shift turnover meetings and observations of daily plant status meetings

to determine whether the equipment configurations were properly listed. The inspectors

also verified that protected equipment was identified and controlled as appropriate and

that significant aspects of plant risk were communicated to the necessary personnel.

16

Enclosure

The reviews of maintenance risk assessment and emergent work evaluation constituted

five inspection procedure samples:

Planned and emergent maintenance during the week of October 15, 2007;

Planned and emergent maintenance during the week of October 22;

Planned and emergent maintenance during the week of October 29;

Planned and emergent maintenance during the week of November 26; and

Planned and emergent maintenance during the week of December 10.

b.

Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1

Service Water (SW) Pump P-32C Issues

a.

Inspection Scope

The inspectors reviewed CAP 01098680, its associated operability evaluation (OPR),

apparent cause evaluation (ACE), and past operability evaluation in the licensees

corrective action program. The inspectors reviewed design basis information, the FSAR,

TS requirements, and licensee procedures to determine the technical adequacy of the

operability evaluations. The inspectors also reviewed the licensees implementation of

select sections of the American Society of Mechanical Engineers (ASME) Operational

Maintenance (OM) Code, 1995 Addenda, to evaluate whether requirements were met

and the appropriate actions were taken in accordance with the Code. In addition, the

inspectors determined whether compensatory measures were implemented, as required.

The inspectors assessed whether system operability was properly justified and that the

system remained available, such that no unrecognized increase in risk occurred.

This review constituted one sample.

b.

Findings

Introduction: A self-revealing finding with no associated violation of regulatory

requirements was identified for an inadequate operability evaluation issued on

June 28, 2007, associated with safety-related SW pump P-32C. Specifically, P-32C

failed its inservice test (IST) on high vibrations after only 6.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of operation, but the

June 2007 operability evaluation had concluded that the pump would remain operable

and not reach the IST out-of-service limit until 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> of continuous operation. The

licensees non-conservative decision-making and use of a non-conservative prediction

model led to the incorrect conclusion of operability of the P-32C pump. Had the licensee

used an appropriate prediction model, reflective of a degraded/degrading pump, the

OPR would have concluded the pump was inoperable.

Description: Service water pump P-32C was placed on increased IST frequency after

trending into the IST Alert Range in May 2007. On June 24, 2007, during the next

performance of increased frequency testing, P-32C vibration was recorded at 0.3051

inches per second (ips) compared to the Required Action limit of > 0.327 ips. Because

this vibration measurements approaching this out-of-service limit of the pump,

17

Enclosure

OPR 01098680 was performed to: review the vibration trend and determine the

additional run time until the IST out-of-service limit might be reached, compare this

duration to the mission time of the P-32C pump, and determine if any additional

compensatory measures were required to be taken.

Licensee engineers utilized vibration analysis software to predict the point at which

P-32C would exceed the 0.327 ips out-of-service limit. Based on the licensees

assumption that the degrading vibration trend was due to normal bearing wear, the trend

projection grossly overestimated the pumps remaining acceptable run time.

Specifically, the model predicted that an additional 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br />, or five days, of continuous

operation could be achieved before reaching 0.327 ips. On August 8, 2007, however,

the next increased frequency IST was performed on P-32C and a vibration level of

0.4055 ips was observed. Because this value exceeded the 0.327 ips IST out-of-service

limit, P-32C was declared inoperable and the appropriate TS action statement was

entered. The pump was subsequently rebuilt and returned to service on August 11 after

71 hours8.217593e-4 days <br />0.0197 hours <br />1.173942e-4 weeks <br />2.70155e-5 months <br /> of unavailability.

The inspectors reviewed ACE 01098680-02. The purpose of this ACE was to determine

the cause of the unexpected step change in vibrations and to determine why vibrations

exceeded the IST out-of-service limit in only 6.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> vice the 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> of predicted

run time. From the review, the inspectors concluded that the licensee applied non-

conservative assumptions to the vibration trend projection when it failed to factor in

vibration amplifying resonance effects, or any additional conservative margin for

uncertainty.

The inspectors identified another example of the licensees non-conservative

decision-making. Specifically, the licensees OPR did not conservatively address

the 30-day design basis mission time of the SW pumps when the IST out-of-service

limit was predicted to be reached in less than the full 30-day mission time.

Section ISTB 6.2.2 of the Code states: If the measured test parameter values fall

within the required action range, the pump shall be declared inoperable until either

the cause of the deviation has been determined and the condition is corrected, or an

analysis of the pump is performed and new reference values are established in

accordance with paragraph ISTB 4.6. of the Code. The licensee did not declare

P-32C inoperable when it was identified that the vibration parameters would exceed the

required action limit within the 30-day mission time of the pump, nor were new baseline

values established in accordance with the Code.

Analysis: The inspectors determined that the failure to use appropriate, conservative,

calculation assumptions in the trend projection to justify the basis for the continued

operability of a safety-related-pump, is a performance deficiency and a finding. The

finding is more than minor because it could reasonably be viewed as a precursor to a

significant event.

Using IMC 0609, Significance Determination Process, dated January 10, 2008, the

inspectors determined that the finding is of very low safety significance (Green) because

the finding did not involve a design deficiency, there was no actual loss of safety

function, no single train loss of safety function for greater than the TS-allowed outage

time, and no risk due to external events.

18

Enclosure

Additionally, the inspectors determined that the finding had a cross-cutting aspect in the

area of human performance. Specifically, the licensee failed to use conservative

assumptions in making decisions affecting the operability of safety-related components

(H.1(b)).

Enforcement: The failure to perform an adequate operability evaluation, which was

based upon non-conservative decision-making and a non-conservative trend projection,

was not a violation of regulatory requirements although a performance deficiency

existed. Therefore, this issue is considered a finding of very low safety significance

(FIN 05000266/2007005-02; 05000301/2007005-02).

The licensee included this finding in its corrective action program as CAP 01119241 and

has actions planned to perform an ACE to address the use of IST trend data in OPRs.

.2

Operability Evaluations for the Unit 2 TDAFW Pump 2P-29 Following Overhaul

a.

Inspection Scope

The inspectors reviewed selected immediate operability evaluations and operability

evaluations associated with issues entered into the licensees corrective action program.

The inspectors reviewed design basis information, the FSAR, TS requirements, and

licensee procedures to determine the technical adequacy of the operability evaluations.

In addition, the inspectors determined whether compensatory measures were

implemented, as required. The inspectors assessed whether system operability was

properly justified and that the system remained available, such that no unrecognized

increase in risk occurred.

The reviews of the following OPRs constituted six samples:

CAP 01112660, 2P-29 Outboard Bearing Water Following IT-09A, dated

September 24, 2007;

CAP 01113318, IT-09A Oil Analysis Results Not as Expected for 2P-29, dated

September 27, 2007;

OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,

Revision 2, dated November 3, 2007;

OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,

Revision 3, dated November 4, 2007;

OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,

Revision 4, dated November 7, 2007; and

OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing,

Revision 5, dated November 10, 2007.

b.

Findings

Introduction: The inspectors identified a finding of very low safety significance (Green)

and an associated Non-Cited Violation of 10 CFR Part 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, for the failure to adequately assess operability

of the Unit 2 TDAFW pump in accordance with plant procedures. The inspectors

identified that the licensee failed to implement procedural requirements regarding the

immediate assessment of operability on September 24 and September 27, 2007, for the

19

Enclosure

increased water ingress into the turbine outboard bearing housing for the pump following

maintenance.

Description: On September 24, 2007, following the overhaul of the 2P-29 TDAFW

pump, an oil sample was taken from the outboard bearing housing, after a four-hour

run. CAP 01112660 was written, which documented that an estimated water volume in

the oil sample based on visual indication was approximately 1,000 to 1,500 parts per

million (ppm) for the four-hour run. The CAP description concluded that this was an

expected condition. A second shorter pump run was performed and the water content in

the oil was visually estimated to be approximately 100 ppm of water. The licensee

rationalized that the initial water content was expected and the condition report was

closed with no further actions taken. However, the inspectors identified that neither the

operations nor engineering staff questioned why a visual estimate for indication of water

in the oil would have produced five times the amount of water in the oil immediately

following the overhaul, as compared to the first oil sample taken in June 2007 following a

November 2006 overhaul, which showed 300 ppm water in the oil. The June 2007

outboard oil sample for the 2P-29 turbine was the first time the oil was sampled since the

November 2006 overhaul and the first time water ingress was noted in the turbine

outboard bearing.

On September 27, CAP 01113318 was written and documented that the outboard oil

sample from the first four-hour run, analyzed by a laboratory, contained 20,040 ppm of

water (approximately two percent by volume). The CAP description also noted that the

number was not consistent with the visual estimate from September 24 of 1,000 to

1,500 ppm. However, the CAP dismissed the results, based on conjecture, concluding

that the 20,040 ppm results were false readings due to a laboratory error or an

accidental capture of water droplets during the sampling process. The CAP concluded

that the indicated levels of water in the IT-09A sample are errant. The immediate

operability assessment concluded that based on the information provided in the

description section there were no operability concerns. In addition, the assessment

discussed that the pump was tested satisfactorily, with no abnormal indications observed

during the run. The inspectors, as well as the licensee personnel performing the causal

evaluation for this issue, concluded that the increased water first observed on

September 24 should not have been discounted and was discounted due to

confirmational biases, resulting in nonconservative assumptions in the evaluation of this

condition.

The inspectors reviewed the licensees procedure for operability, Fleet Procedure

FP OP-OL-01, Operability Determination. The procedure required a determination if

a condition existed that could call into question the ability of a structure, system, or

component (SSC) to perform its specified safety function. An example of such a

condition was an item which met the definition of a degraded condition. A degraded

condition, as defined in the fleet procedure, was a condition where there had been a

noticeable change in parameters that were precursors to failure. The attachment

guidance for immediate operability review also highlighted questions for performing

operability determinations, which included the following: Could the capability of a SSC

to prevent or mitigate consequences of an accident as postulated in the Final Safety

Analysis Report be reduced? The guidance suggested that an OPR should be

requested if additional engineering evaluation and justification was needed to answer

those questions. Finally, the inspectors noted that the guidelines for operability

recommendations included guidance to evaluate trend data to identify a deteriorating

20

Enclosure

condition and to utilize an OPR to predict the point when a SSC may become

inoperable. The inspectors concluded the licensee had not adequately implemented the

procedures for operability determinations for the September 24 and 27 CAPs. The

licensee had not assessed the parameter of a significant increase in the ingress of water

following a maintenance overhaul, as compared to the last maintenance overhaul.

On November 1, 2007, approximately 5 weeks after the maintenance overhaul, the

licensee ran 2P-29 for about two hours and then sampled the oil. The outboard oil

sample had 29,515 ppm of water in the oil. The licensee declared the pump inoperable

and revised the July 2007 operability evaluation for the original water ingress issue in

June.

On November 3, the licensee issued Revision 2 to OPR1098358 and the pump was

determined to be capable of performing the design functions for the design basis mission

time of eight hours. On November 4, Revision 3 to OPR1098358 was issued to specify

a compensatory measure of testing the pump every 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> for an eight-hour duration.

The subsequent pump runs continued to show high levels of water in the outboard

bearing oil. The inspectors identified that Revisions 2 and 3 utilized data from 2P-29 on

water ingress rates prior to the September 2007 turbine overhaul. These values were

not applicable to the current condition, because the September maintenance had

created a new and greater water ingress problem. Revision 4 to OPR1098358, issued

on November 7, was a rewrite of the OPR utilizing current oil analysis data from after the

overhaul. In addition, the licensee hypothesized, as part of the operability discussion,

that differences in water concentrations in the oil seen since November 1 were likely the

result of a change in sampling techniques. However, the inspectors noted that these

theories were refuted by visual observation and comparison of the quarantined oil

samples taken since November 1. Further testing of the previous oil samples also

refuted the sampling technique theories. In addition, the inspectors noted that the

licensee did not have any established procedural controls or work instructions for mixing

of the samples and splitting of the samples to ensure quality control. The licensee

initiated a condition report and took immediate corrective actions to address this latter

issue. Revision 5 to the OPR was issued on November 10 and contained additional

discussion on the potential for an unexpected increase in steam leakage, and additional

information related to the sampling technique and testing duration.

The inspectors noted that for all the revisions, the OPR demonstrated that the TDAFW

pump would have performed the required safety functions for the eight-hour mission time

of the FSAR Chapter 14 design basis accidents. However, the inspectors pointed out to

the licensee that the OPR did not address all the safety functions required to be

performed by the TDAFW pump, which at Point Beach included several fire-related

scenarios. The licensee subsequently initiated a CAP for this issue.

Additional information regarding the issues associated with the 2P-29 TDAFW pump is

documented in Section 4OA5.2 of this report.

Analysis: The inspectors determined that the failure to adequately perform an operability

determination was a performance deficiency and a finding that warranted a significance

evaluation. Using IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, dated September 20, 2007, the inspectors determined that the finding is

more than minor because, if left uncorrected, the failure to properly assess operability

21

Enclosure

would result in the TDAFW pump being degraded and potentially inoperable, exceeding

the allowed outage time in accordance with TSs.

Using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection

Findings for At-Power Situations, dated January 10, 2008, the inspectors determined

the finding may have resulted in a late determination of an actual loss of safety function

of a system or train of equipment. The risk assessment for the potential loss of safety

function is attributed to the performance deficiencies associated with inadequate

maintenance discussed in Section 4OA5.2.b.2 as URI 5000266/2007005-07. This did

not cause the loss of safety function for greater than the allowed outage time.

Therefore, the finding is considered to be of very low safety significance (Green).

Additionally, the inspectors determined that the finding has a cross-cutting aspect in the

area of human performance. Specifically, the licensee failed to use conservative

assumptions in decision-making affecting operability of safety-related equipment

(H.1(b)).

Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality be prescribed and

accomplished by procedures appropriate to the circumstances. The licensee failed

to implement the operability determination procedure FP-OP-OL-01, Operability

Determination. The procedure required, in part, that the licensee assess the

capability of a SSC to prevent or mitigate consequences of an accident as

postulated in the FSAR. Contrary to this, the licensee failed to adequately assess

the operability of the turbine outboard bearing for the Unit 2 TDAFW pump following

increased water intrusion during post-maintenance testing on September 24, 2007,

and later corroborated by oil analyses on September 27. Because this finding was of

very low safety significance (Green) and because it was entered into the licensees

corrective action program (as CAP 01115748), this violation is being treated as a

Non-Cited Violation, consistent with Section VI.A of the NRC Enforcement Policy

(NCV 05000301/2007005-03).

The licensee took immediate corrective actions to address the issue, and at the end of

the inspection period the licensee continued to evaluate the causes associated with this

finding.

.3

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed selected operability evaluations associated with issues entered

into the licensees corrective action program. The inspectors reviewed design basis

information, the FSAR, TS requirements, and licensee procedures to determine the

technical adequacy of the operability evaluations. In addition, the inspectors determined

whether compensatory measures were implemented, as required. The inspectors

assessed whether system operability was properly justified and that the system

remained available, such that no unrecognized increase in risk occurred.

22

Enclosure

The reviews of the following operability evaluations constituted four samples:

CAP 00889745, Degraded Grid Voltage Concerns;

CAP 01111251, Discrepancy in Control Room Accident Fan Brake Horsepower

Versus Vendor Data Used in Calculation 2004-0002, Revision 6;

CAP 01114308, Unit 1 and 2 Safety Injection Valves 850A/B, Sump B Suction

Valve Limit Switches; and

CAP 01116453, Unit 2 W-3B Control Rod Drive Shroud Fan Tripped on

Overcurrent.

b.

Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17)

.1

Annual Resident Review

a.

Inspection Scope

The following engineering design package was reviewed and selected aspects were

discussed with engineering personnel:

EDG G-01 and G-02 heat exchanger modification

This document and related documentation were reviewed to assess adequacy of the

associated 10 CFR 50.59 safety evaluation screening; consideration of design

parameters; implementation of the modification; post-modification testing, and proper

updating of procedures, design, and licensing documents. The inspectors observed

ongoing and completed work activities to verify that installation was consistent with the

design control documents. The modifications were installed to address a longstanding

operator workaround for lake grass fouling of the heat exchangers.

This inspection constituted one sample.

b.

Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

a.

Inspection Scope

During completion of the post-maintenance test inspection procedure samples, the

inspectors observed in-plant activities and reviewed procedures and associated records

to determine whether:

Testing activities satisfied the test procedure acceptance criteria;

Effects of the testing were adequately addressed prior to the testing;

Measuring and test equipment calibration was current;

Test equipment was within the required range and accuracy;

23

Enclosure

Applicable prerequisites described in the test procedures were satisfied;

Affected systems or components were removed from service in accordance with

approved procedures;

Testing activities were performed in accordance with the test procedures and

other applicable procedures;

Jumpers and lifted leads were controlled and restored where used;

Test data and results were accurate, complete, and valid;

Test equipment was removed after testing;

Equipment was returned to a position or status required to support the operability

of the system in accordance with approved procedures; and

All problems identified during the testing were appropriately entered into the

corrective action program.

The activities listed below were reviewed by the inspectors and constituted three

quarterly inspection procedure samples:

Unit 1 Charging Pump P-2A;

Unit 1 Charging Pump P-2B Variable Frequency Drive; and

Service Water Pump P-32E.

b.

Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

During completion of the inspection procedure samples, the inspectors observed in-plant

activities and reviewed procedures and associated records to determine whether:

Preconditioning occurred;

Effects of the testing were adequately addressed by control room personnel or

engineers prior to the commencement of the testing;

Acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

Plant equipment calibration was correct, accurate, and properly documented; as-

left setpoints were within required ranges; and the calibration frequency were in

accordance with TSs, the FSAR, procedures, and applicable commitments;

Measuring and test equipment calibration was current;

Test equipment was used within the required range and accuracy;

Applicable prerequisites described in the test procedures were satisfied;

Test frequencies met TS requirements to demonstrate operability and reliability;

Tests were performed in accordance with the test procedures and other

applicable procedures;

Jumpers and lifted leads were controlled and restored where used;

Test data and results were accurate, complete, within limits, and valid;

Test equipment was removed after testing;

24

Enclosure

Where applicable for IST activities, testing was performed in accordance with the

applicable version of Section XI, American Society of Mechanical Engineers

Code, and reference values were consistent with the system design basis;

Where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

Where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

Where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

Prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

Equipment was returned to a position or status required to support the

performance of its safety functions; and

All problems identified during the testing were appropriately documented and

dispositioned in the corrective action program.

During this inspection period, the inspectors completed the following inspection

procedure samples, which included two routine surveillances, two inservice tests, and

one containment isolation valve test, for a total of five quarterly inspection procedure

samples:

EDG G01 surveillance testing during the week of October 22, 2007;

Unit 2 TDAFW pump 2P-29 ISTs on November 1 and 2;

Unit 2 TDAFW pump 2P-29 ISTs on November 7;

EDG G02 surveillance testing during the week of November 11; and

Testing of Unit 2 containment isolation valve SC-966.

b.

Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a.

Inspection Scope

The inspectors reviewed the following temporary modification:

Furmanite injection of Unit 2 Moisture Separator Reheater Purge

Valve 2MS-32A.

The inspectors compared the temporary configuration changes and associated

10 CFR 50.59 screening and evaluation information against the design basis, the FSAR,

and the TS, as applicable, to verify that the modification did not affect the operability or

availability of the affected system. The inspectors also compared the licensees

information to operating experience information to ensure that lessons learned from

other utilities had been incorporated into the licensees decision to implement the

temporary modification. The inspectors, as applicable, performed field verifications to

ensure that the modifications were installed as directed; the modifications operated as

expected; modification testing adequately demonstrated continued system operability,

25

Enclosure

availability, and reliability; and that operation of the modifications did not impact the

operability of any interfacing systems. Lastly, the inspectors discussed the temporary

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how extended operation with the temporary modification in

place could impact overall plant performance.

This inspection constituted one sample.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

The inspectors performed a screening review of the 2006 and 2007 revisions to the

Point Beach Emergency Plan Manual to determine whether the changes decreased the

plans effectiveness. This review did not constitute an approval of the changes, and as

such, the changes are subject to future NRC inspection to ensure that the emergency

plan continues to meet NRC regulations.

These activities completed one inspection sample.

b.

Findings

No findings of significance were identified

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03)

.1

Inspection Planning

a.

Inspection Scope

The inspectors reviewed the FSAR to identify applicable radiation monitors associated

with measuring transient high and very high radiation areas, including those intended for

remote emergency assessment. The inspectors identified the types of portable radiation

detection instrumentation used for job coverage of high radiation area work, including

instruments used for underwater surveys, portable and fixed area radiation monitors

used to provide radiological information in various plant areas, and continuous air

monitors used to assess airborne radiological conditions and, consequently, work areas

with the potential for workers to receive a 50 millirem or greater committed effective dose

equivalent (CEDE). Whole body counters used to monitor for internal exposure and

those radiation detection instruments utilized to conduct surveys for the release of

personnel and equipment from the radiologically controlled area (RCA), including

contamination monitors and portal monitors, were also identified.

26

Enclosure

These reviews represented two inspection samples.

b.

Findings

No findings of significance were identified.

.2

Walkdowns of Radiation Monitoring Instrumentation

a.

Inspection Scope

The inspectors conducted walkdowns of selected area radiation monitors (ARMs) in the

Unit 1 and Unit 2 auxiliary building to determine if these monitors were located and

provided measurement capability as described in the FSAR and were optimally

positioned relative to the potential sources of radiation they were intended to monitor.

Walkdowns were conducted of those areas where portable survey instruments were

source checked and maintained for radiation protection (RP) staff use to determine if

those instruments designated ready for use were sufficient in number to support the

RP program, had current calibration stickers, were operable, and were in adequate

physical condition. Also, the inspectors observed the licensees portable survey

instrument calibration units and the radiation sources used for operability checks of

various radiation measuring instruments to assess their material condition and discussed

their use with RP staff to determine if they were used appropriately. Additionally, the

inspectors observed the use of the instrument calibration units, discussed with the staff

calibrator output validation methods, and compared calibrator exposed readings with

calculated/expected values. The inspectors evaluated compliance with licensee

procedures while RP personnel demonstrated the methods for performing source checks

of portable survey instruments and source checks of personnel contamination and portal

monitors located at the egress to the RCA and the plant protected area.

These reviews represented one partial inspection sample, which combined with

Section 2OS3.3 constituted one sample.

b.

Findings

No findings of significance were identified.

.3

Calibration and Testing of Radiation Monitoring Instrumentation

a.

Inspection Scope

The inspectors selectively reviewed radiological instrumentation associated with

monitoring transient high and/or very high radiation areas, instruments used for remote

emergency assessment, and radiation monitors used to identify personnel contamination

and for assessment of internal exposures to verify that the instruments had been

calibrated as required by the licensees procedures, consistent with industry and

regulatory standards. The inspectors also reviewed alarm setpoints for selected ARMs,

for personnel contamination monitors and for portal (egress) monitors to verify that they

were established consistent with the FSAR or TSs, as applicable, and were consistent

with industry practices and regulatory guidance. Specifically, the inspectors reviewed

calibration procedures and the most recent calibration records for the following radiation

monitoring instrumentation and calibration equipment:

27

Enclosure

Unit 1 and Unit 2 Containment High Range (Accident) Radiation Monitors;

Unit 1 and Unit 2 Charging Pump Room Low and High Range ARMs;

Unit 1 and Unit 2 Seal Table ARMs;

Unit 1 and Unit 2 Post-Accident Sample Line Monitors;

Common Unit Safety Injection Pump Room Low and High Range ARMs;

Portable Gamma and Neutron Survey Instruments (Model AMP-100 and ASP-1);

Portable Air Sampler (Model AMS-4);

Portal (Gamma) Monitors Used at RCA and Protected Area Egresses;

Personnel Contamination Monitors Used at RCA Egress;

Two Instrument Calibrators (and the associated instruments used to measure

calibrator output); and

Whole Body Counter.

The inspectors determined what actions were taken when, during calibration or source

checks, an instrument was found significantly out of calibration or exceeded as-found

acceptance criteria. Should that occur, the inspectors verified that the licensees actions

would include a determination of the instruments previous uses and the possible

consequences of that use since the prior calibration. The inspectors also reviewed the

results of the licensees most recent 10 CFR Part 61 source term (radionuclide mix)

evaluation to determine if instrument/monitor calibration and check sources were

representative of the plant source term. Given that source term, the inspectors reviewed

the licensees method for internal dose assessment to determine if difficult to detect

nuclides were scaled into whole body count dose determinations.

These reviews represented one partial inspection sample, which combined with

Section 2OS3.2 constituted one sample.

b. Findings

No findings of significance were identified.

.4

Problem Identification and Resolution

a.

Inspection Scope

The inspectors reviewed corrective action documents and any special reports that

involved personnel contamination monitor alarms due to personnel internal exposures to

determine whether identified problems were entered into the corrective action program

for resolution. Licensee self-assessments, audits, and corrective action documents were

also reviewed to determine if problems with radiological instrumentation or with self-

contained breathing apparatus (SCBA) were identified, characterized, prioritized, and

resolved effectively using the corrective action program.

While no internal exposure with a CEDE greater than 50 millirem occurred since the last

inspection in this area, the inspectors reviewed the licensees methodology for internal

dose assessment.

The inspectors reviewed corrective action program reports related to exposure-

significant radiological incidents that involved radiation monitoring instrument

deficiencies since the last inspection in this area, as applicable. Members of the RP

staff were interviewed and corrective action documents were reviewed to determine

28

Enclosure

whether follow-up activities were being conducted in an effective and timely manner

commensurate with their importance to safety and risk based on the following:

Initial problem identification, characterization, and tracking;

Disposition of operability/reportability issues;

Evaluation of safety significance/risk and priority for resolution;

Identification of repetitive problems;

Identification of contributing causes;

Resolution of Non-Cited Violations tracked in the corrective action program; and

Identification and implementation of effective corrective actions.

The inspectors determined if the licensees self-assessment and audit activities

completed for the approximate two-year period that preceded the inspection were

identifying and addressing repetitive deficiencies or significant individual deficiencies in

problem identification and resolution, as applicable.

These reviews represented three inspection samples.

b.

Findings

No findings of significance were identified.

.5

RP Technician Instrument Use

a.

Inspection Scope

The inspectors selectively determined whether calibrations for those survey instruments

used to perform job coverage surveys and for those currently designated for use had not

lapsed. The inspectors reviewed instrument issue logs for selected dates in 2007 to

determine if response checks of portable survey instruments and checks of instruments

used for unconditional release of materials and workers from the RCA were completed

prior to instrument use, or daily, as required by the licensees procedure. The inspectors

also discussed instrument calibration methods and source response check practices

with radiation protection staff and observed staff demonstrate instrument source checks.

These reviews represented one inspection sample.

b.

Findings

No findings of significance were identified.

.6

SCBA Maintenance/Inspection and Emergency Response Staff Qualifications

a.

Inspection Scope

The inspectors reviewed aspects of the licensees respiratory protection program for

compliance with the requirements of Subpart H of 10 CFR Part 20 and to determine if

SCBA equipment was properly inspected, maintained, and ready for emergency use.

The inspectors reviewed records of inspection and functional tests performed in 2006

and 2007 for all SCBAs staged in the plant to support both the licensees fire brigade

and emergency response organization, as provided in the Point Beach Emergency Plan.

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Enclosure

The inspectors evaluated the licensees capabilities for refilling and transporting SCBA

air bottles to and from the control room during emergency conditions. The inspectors

determined if control room staff designated for the active on shift duty roster were

trained, respirator fit-tested, and medically certified to use SCBAs. Additionally, the

inspectors reviewed SCBA qualification records for the licensees radiological

emergency teams, including the radiation protection, chemistry, and maintenance staffs,

to determine if a sufficient number of staff were qualified to fulfill emergency response

positions consistent with the Emergency Plan and the requirements of 10 CFR 50.47.

The inspectors also reviewed the respiratory protection training lesson plan to assess its

overall adequacy relative to Subpart H of 10 CFR Part 20.

The inspectors walked down SCBA equipment maintained in the control room, the

Operations Support Center, various areas of the turbine building and in the warehouse

fire brigade ready rooms, as well as spare SCBA air bottle stations. During these

walkdowns, the inspectors examined numerous SCBA units to assess their material

condition and to determine if air bottle hydrostatic tests were current and if bottles were

pressurized to meet procedural requirements. The inspectors reviewed records of

SCBA equipment inspection and functional testing, including results of the most recent

regulator flow tests for all SCBA units maintained at the site. Additionally, the inspectors

observed members of the licensees operations and RP staffs demonstrate the methods

used to conduct the inspections and functional tests to determine if these activities were

performed consistent with procedure and the equipment manufacturers

recommendations. The inspectors also evaluated through record review and

observations if the required air cylinder hydrostatic testing was documented and current,

if the Department of Transportation required retest air cylinder markings were in place

for numerous randomly selected SCBA units and spare air bottles, and if air quality for

the compressor used to fill SCBA air bottles was routinely tested to verify Grade-D

quality. The inspectors also reviewed the qualification documentation (training

certificate) issued by the SCBA manufacturer to an individual contracted by the licensee

to perform maintenance/repair of SCBA vital components. Pressure regulator test/repair

records for 2007 for all SCBA units designated for emergency use were reviewed to

determine if the equipment was adequately maintained consistent with the

manufacturers maintenance procedure.

These reviews represented two inspection samples.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

.1

Data Submission Issue

a.

Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the 4th

quarter 2007 PIs for any obvious inconsistencies prior to its public release in accordance

with IMC 0608, Performance Indicator Program.

30

Enclosure

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b.

Findings

No findings of significance were identified.

.2

Mitigating Systems Performance Index - Emergency AC Power System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) Emergency AC Power System PIs, for both Units, for July 2006 through

March 2007. To determine the accuracy of the data the inspectors used definitions and

guidance in Revision 5 of the Nuclear Energy Institute (NEI) Document 99-02,

Regulatory Assessment Performance Indicator Guideline. The inspectors reviewed the

licensees operator narrative logs, MSPI derivation reports, issue reports, event reports,

and NRC integrated inspection reports for July 1, 2006, to March 31, 2007, to validate

the accuracy of the submittals. The inspectors reviewed the MSPI component risk

coefficient to determine if it had changed by more than 25 percent since the previous

inspection, and if so, that the change was in accordance with applicable NEI guidance.

The inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the PI data collected or transmitted for this indicator;

were identified.

This inspection constituted two MSPI emergency AC power system samples.

b.

Findings

No findings of significance were identified.

.3

Mitigating Systems Performance Index - High Pressure Injection Systems

a.

Inspection Scope

The inspectors sampled licensee submittals for the MSPI - High Pressure Injection

Systems PIs, for both Units, for July 2006 through March 2007. To determine the

accuracy of the PI data the inspectors used definitions and guidance contained in

NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue

reports, MSPI derivation reports, event reports, and NRC integrated inspection reports

for July 1, 2006 to March 31, 2007, to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified.

This inspection constituted two MSPI high pressure injection system samples.

31

Enclosure

b.

Findings

No findings of significance were identified.

.4

Mitigating Systems Performance Index - Heat Removal System

a.

Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Heat Removal System PI, for

both Units, for July 2006 through March 2007. To determine the accuracy of the PI data

reported during that period, the inspectors used PI definitions and guidance in

NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue

reports, event reports, MSPI derivation reports, and NRC integrated inspection reports

for July 1, 2006, to March 31, 2007, to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified.

This inspection constituted two MSPI heat removal system samples.

b.

Findings

No findings of significance were identified.

.5

Mitigating Systems Performance Index - Residual Heat Removal System

a.

Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Residual Heat Removal

System PI, for both Units, for July 2006 through March 2007. To determine the accuracy

of the PI data reported during that period the inspectors used definitions and guidance in

NEI 99-02. The inspectors reviewed the licensees operator narrative logs, issue

reports, MSPI derivation reports, event reports, and NRC integrated inspection reports

for July 1, 2006, to March 31, 2007, to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

This inspection constituted two MSPI residual heat removal system samples.

b.

Findings

No findings of significance were identified.

32

Enclosure

.6

Mitigating Systems Performance Index - Cooling Water Systems

a.

Inspection Scope

The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems PI for

July 2006 through March 2007. To determine the accuracy of the PI data reported

during those periods, the inspectors used definitions and guidance in NEI 99-02. The

inspectors reviewed the licensees operator narrative logs, issue reports, MSPI

derivation reports, event reports, and NRC integrated inspection reports for July 1, 2006,

to March 31, 2007, to validate the accuracy of the submittals. The inspectors reviewed

the MSPI component risk coefficient to determine if it had changed by more than

25 percent since the previous inspection, and if so, that the change was in accordance

with applicable NEI guidance. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified.

This inspection constituted two MSPI cooling water system samples.

b.

Findings

No findings of significance were identified.

.7

Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent

Occurrences

a.

Inspection Scope

The inspectors used definitions and guidance contained in Revision 5 of NEI 99-02

to verify the accuracy of the data for the Radiological Effluent Technical

Specification/Offsite Dose Calculation Manual (RETS/ODCM) Radiological Effluent

Occurrence PI.

The inspectors reviewed the licensees CAP database and selected individual condition

reports generated between December 2006 and November 2007 to identify any potential

occurrences such as unmonitored, uncontrolled, or improperly calculated effluent

releases that may have impacted offsite dose. The inspectors also selectively reviewed

gaseous and liquid effluent summary data and the results of associated offsite dose

calculations for selected periods in 2007 to determine if indicator results were accurately

reported. The inspectors also discussed with the licensee the methods for quantifying

gaseous and liquid effluents and for determining effluent dose.

These reviews represented one inspection sample.

b. Findings

No findings of significance were identified.

33

Enclosure

4OA2 Problem Identification and Resolution (71152)

.1

Routine Resident Inspector Review

a.

Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed

issues during baseline inspection activities and plant status reviews to determine

whether issues were entered into the licensees corrective action program at an

appropriate threshold, that adequate attention was given to timely corrective actions, and

that adverse trends were identified and addressed. The inspectors also reviewed all

CAPs written during the inspection period. The CAPs written by the licensee as a result

of inspectors observations are included in the list of documents in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

.2

Selected Issue Follow-up Inspection: Annual Review of Operator Workarounds

Introduction

The inspectors selected operator workarounds for a more in-depth review in accordance

with Inspection Procedure requirements.

This annual review of operator workarounds constituted one inspection sample.

a.

Effectiveness of Problem Identification

(1) Inspection Scope

The inspectors reviewed plant logs, condition reports, and work requests to verify that

the licensees identification of operator workarounds was complete, accurate, and timely,

and that the consideration of extent of condition review, generic implications, common

cause, and previous occurrences was adequate.

(2) Findings and Issues

No findings of significance were identified. No issues were identified.

b.

Prioritization and Evaluation of Issues

(1) Inspection Scope

The inspectors reviewed plant logs, condition reports, and work requests associated with

existing operator burdens, including operator workarounds, operator challenges, and

control room deficiencies. The nature and significance of individual issues and all issues

in aggregate with respect to safety, risk, and licensee corrective action procedural

requirements were considered. Additionally, the inspectors assessed the licensees

evaluation and disposition of performance issues, evaluation and disposition of

operability issues, and application of risk insights for prioritization of issues.

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Enclosure

(2) Findings and Issues

No findings of significance were identified. No issues were identified.

c.

Effectiveness of Corrective Actions

(1) Inspection Scope

The inspectors reviewed condition reports and work requests associated with existing

operator workarounds, operator challenges, and control room deficiencies to determine if

the licensees corrective action program addressed generic implications. Additionally,

the inspectors verified that established corrective actions by the licensee were

appropriately focused to correct the problem.

(2) Findings and Issues

No findings of significance were identified. No issues were identified.

.3

Semiannual Trend Review

a.

Inspection Scope

The inspectors reviewed of the licensees CAPs and associated documents to identify

trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered July 2007 through December 2007, although some

examples expanded beyond those dates.

The reviews also included issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.

The inspectors compared and contrasted their results with the results contained in the

licensees corrective action program trending reports. Corrective actions associated with

a sample of the issues identified in the licensees trending reports were reviewed for

adequacy.

This semi-annual trend review by the inspectors constituted one inspection.

b.

Findings and Issues.

No findings of significance were identified. No issues were identified.

35

Enclosure

4OA3 Followup of Events and Notices of Enforcement Discretion (71153)

.1

TS-Required Shutdown Due to High Unit 2 Refueling Water Storage Tank Temperature

a.

Inspection Scope

Through record reviews and discussion with plant staff, the inspectors assessed the

circumstances of a TS-required shutdown initiated on September 18, 2007. Although

the licensee took immediate corrective actions to de-energize the submersion heaters

and cool the RWST by forced recirculation, the temperature could not be restored to

acceptable limits before the eight-hour TS action statement expired. As a result, Unit 2

commenced a TS-required shutdown that was later averted, while at approximately

20 percent reactor power, when the RWST temperature was restored to within

acceptable limits. The inspection scope included a review of the events leading up to

the shutdown initiation.

b. Findings

Introduction: A self-revealing finding of very low safety significance (Green) and an

associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, was identified for the failure to allow operators

to properly set the thermostat of the Unit 2 RWST heaters, and to ensure that the RWST

was recirculated frequently enough for the temperature indicator to accurately measure

bulk temperature.

Description: On September 18, 2007, during the performance of TS-required

surveillance SR 3.5.4.1, the Unit 2 RWST was found to be at 105 °F. The TS

maximum allowable limit was 100 °F (97 °F parametric). Because RWST temperature

could not be restored within the allowed eight hours, operators commenced a shutdown

of Unit 2. At 20 percent power, the temperature was returned to within acceptable limits

and the operators began to raise reactor power to 100 percent. The cause of the

elevated temperature was found to be the incorrectly set RWST heater thermostat.

It was identified that on August 30, the controlling thermostat for the RWST heaters was

incorrectly set to 95 °F vice 50 °F as required by procedure. For the 18 days between

August 30 and September 18, the bulk water temperature increased to 105 °F through

natural circulation. During this period, daily temperature readings of the RWST only

showed an increase from 75 °F to 85 °F. This disparity occurred due to stratification

caused by the location of the single temperature indicator relative to the heaters inside

the tank. Because the RWST temperature indicator is located 2 feet from the bottom of

the 70 foot tall tank, and the heaters are located 4.5 feet above the indicator,

stratification caused the temperature indicator to remain in a layer of colder water. It

was not until September 18, that the RWST temperature was found to be at 105 °F, after

four hours of being on forced recirculation.

The inspectors reviewed procedure PC 49, part 4, Revision 19, which was used for

setting the thermostat on the RWSTs to 50 °F. This task was performed once a year

during cold weather preparations to ensure that the RWST remained within the required

temperature range of 40 to 100 °F. Through this review, the inspectors concluded that a

lack of sufficient detail existed for the critical step of setting the thermostat, which directly

affected the operability of the safety-related RWST. Specifically, the lack of procedural

36

Enclosure

detail contributed to the operators reliance upon an unapproved operator aid in the field;

in this case, a black marking that was believed by the operator to indicate the desired

thermostat setting.

The inspectors also reviewed procedure PC 25, Revision 23, which was used to

recirculate and purify the RWST. This task was performed to keep the RWST contents

in a homogeneous mixture to prevent stratification. Through this review, the inspectors

concluded that the frequency of RWST recirculation, which was performed monthly, was

inadequate to ensure that the temperature indicator accurately read bulk tank

temperature to satisfy the TS operability requirements, while the heaters were

energized.

Analysis: The inspectors determined that the failure to have adequate procedures in

place to ensure the operability of the safety related RWST is a performance deficiency

and a finding. The finding is more than minor in accordance with IMC 0612, Power

Reactor Inspection Reports, Appendix B, Issue Screening, dated September 20, 2007,

because it is associated with the procedural quality and human performance attributes of

the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring

the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

Using IMC 0609, Significance Determination Process, dated January 10, 2008, the

inspectors determined that the finding is of very low safety significance (Green) because

the finding did not involve a design deficiency, there was no actual loss of safety

function, no single train loss of safety function for greater than the TS allowed outage

time, and no risk due to external events. The inspectors also determined that the finding

had a cross-cutting aspect in the area of human performance. Specifically, human error

prevention techniques were not utilized prior to and during the thermostat setting task

and personnel proceeded in the face of uncertainty and unexpected circumstances

(H.4(a)).

Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances and

shall be accomplished in accordance with these instructions, procedures and drawings.

Contrary to this, the licensees procedure PC 49, part 4, used for setting the RWST

heater thermostat, did not have adequate instructions for correctly setting the

thermostat. Further, the monthly recirculation of the RWST, specified in procedure

PC-25, was not appropriate to ensure that the TS-required temperature readings were

valid in their indication of bulk tank temperature while heaters were energized. Because

of the very low safety significance of this finding and because the finding was entered

into the licensees corrective action program (CAP 01111841), the violation is being

treated as an NCV, consistent with Section VI.A.1 of NRC Enforcement Policy

(NCV 05000266/2007005-04; 05000301/2007005-04).

The licensee entered the event into its corrective unit action program, took corrective

actions to increase the frequency of the Unit 1 and Unit 2 RWST recirculation to once

every seven days until the heaters were no longer needed due to seasonal temperature

increases, and conducted a root cause evaluation.

37

Enclosure

.2

(Closed) Violation (VIO)05000266/2006011-01; 050000301/2006011-01: Failure to

Update Final Safety Analysis Report with Reactor Head Drop Analysis and Obtain NRC

Approval

The inspectors evaluated the licensees corrective action program responses to the

January 29, 2007, Notice of Violation associated with the NRC Special Inspection Report

05000266/2006011; 05000301/2006011, for issues in the spring of 2005, regarding a

1982 reactor vessel head drop analysis. The inspectors reviewed the corrective actions

the licensee described in its correspondence dated December 19, 2006, entitled,

Response to an Apparent Violation in Inspection Report05000266/2006011;

05000301/2006011; EA-06-274. The inspectors validated the following corrective

actions were complete: incorporation of the Reactor Vessel Head Drop Analyses into

the FSAR; revision of the Technical Requirements Manual Section 3.9.4; revision of

plant procedures, including maintenance, outage, and operations procedures and

checklists; development of a licensing basis policy and training for plant staff on that

policy; development and implementation of a continuing training module for plant

engineers; licensee evaluation and validation of commitments contained in an

October 1996 NRC, Request for Information Pursuant to 10 CFR 50.54(f) Regarding

Adequacy and Availability of Design Basis Information, with corresponding corrective

actions for identified deficiencies; and development of a procedure writer/reviewer

certification matrix with a job familiarization guide which addressed how to search the

sites regulatory information system. The review by the inspectors constituted one

inspection procedure sample.

4OA5 Other Activities

.1

(Closed) Unresolved Item (URI) 05000266/2007008-06: Inadequate Post-Maintenance

Testing (PMT) of the Turbine-Driven Auxiliary Feedwater Pumps Following Major

Maintenance

Introduction: The inspectors identified a finding of very low safety significance (Green)

and an associated Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, for the licensees failure to conduct adequate

PMT of the Unit 1 1P-29 TDAFW pump following a ten-year overhaul of the turbine in

May 2007. Specifically, the ten-year overhaul maintenance included bearing

replacement, but, the PMT did not run the TDAFW pump long enough for bearing

temperature to stabilize. The appropriate PMT would have detected that the bearing

temperatures were rising and required evaluation prior to declaring the TDAFW

operable.

Description: The licensee completed an overhaul of the Unit 1 TDAFW turbine and the

associated PMT on May 6, 2007, declaring the TDAFW pump operable following

completion of quarterly IST procedure IT-8A. The PMT requirements for the overhaul

were listed in the maintenance overhaul procedure, RMP 9044-1. The IST procedure

had no specific requirements to monitor bearing temperatures for stabilization other than

to perform the IST, which recorded bearing temperature data. The procedure did have a

temperature limit to place the pump in the alert range and conduct an engineering

evaluation when the turbine outboard bearing exceeded 225 °F, and to remove the

pump from service and declare the pump inoperable when the same bearing exceeded

250 °F. However, as part of the PMT for the ten-year overhaul, there was no

38

Enclosure

requirement in either the work order, maintenance procedure or the IST procedure, to

ensure bearing temperatures were stabilized.

For testing on May 1, the inspectors noted that the outboard bearing temperature

reached 247 °F, as indicated on the chart recorders. During the PMT on May 6, some

licensee personnel noted the turbine outboard bearing rising, but indicated the

temperatures was stabilizing. However, the licensee did not wait for temperature

stabilization and secured the Unit 1 TDAFW pump. The inspectors review of chart

recorders revealed that the outboard bearing temperature was at 238 °F and still rising.

The licensee had declared the TDAFW pump operable with no PMT assessment of the

outboard bearing temperature trend and no engineering analysis or evaluation of the

changes in outboard bearing temperature from prior to the overhaul.

During the Unit 1 TDAFW pump quarterly IST procedure IT-8A performance on June 9,

turbine outboard bearing temperature exceeded 225 °F. The turbine outboard bearing

temperature was at 233 °F and still rising when the pump was secured after the test was

completed. In this case, a CAP was written and a follow-up test was completed on

June 12, with the goal to attain bearing temperature stabilization. The test was stopped

at around 249.5 °F, prior to bearing temperature stabilization, and the 250 °F limit to

secure the pump. The pump was declared inoperable and the plant was subsequently

shutdown to repair the TDAFW turbine.

The licensees root cause evaluation indicated the turbine was improperly assembled

during the overhaul in May 2007. In addition, the inspectors determined that changes to

procedure NP 10.2.7, Post Maintenance/Return to Service Testing, did not occur when

a change in the ASME OM Code in 1998 resulted in removing stabilization criteria from

the normal ISTs for safety-related equipment. Specifically, the procedure allowed credit

to be taken for ISTs; however, the procedure did not alert personnel that ISTs no longer

required temperature stabilization. Procedure NP 10.2.7, did specify that licensee

personnel review the PMT matrix for maintenance tasks performed, and the PMT matrix

specified temperature stabilization for bearing replacements. In addition, the licensee

concluded from the root cause that: people interviewed, who were involved with the

PMT recommendation, approval, and review process rely on the applicable procedure to

be correct and do not verify that the correct PMT is specified in the procedures; many

operations, engineering, and planning personnel rely on memory when assigning PMT to

work that does not have a procedure-based PMT; and additional training may be

necessary for PMT activities.

Past Operability and Availability Analysis

From July through December 2007, the licensee evaluated the past operability and

availability of the Unit 1 TDAFW pump. The inspectors, in conjunction with a technical

matter expert from the Office of Nuclear Reactor Regulation and a Regional Senior

Reactor Analyst, reviewed the licensees past availability analysis, and verified the

assumptions, calculations, and conclusions made by the licensee in AR 01090456, Past

Availability 1P-29 Turbine Driven Auxiliary Feedwater Pump. The inspectors verified

the conclusion made by the licensee that the as-found condition of the turbine would

have resulted in the turbine being able to perform its function for the 24-hour mission

time. The as-found condition consisted of the following known deficiencies caused by

the spring 2007 maintenance: inadequate wheel lap setting, inadequate pump-to-turbine

coupling stretch; inadequate stretch and misalignment in the gear box coupling; and

39

Enclosure

inadequate thrust bearing axial end clearance. The basis for concluding that the

TDAFW pump would have performed its function were as follows: the accumulated run

time without component degradation provided indications of satisfactory operation of

components other than the bearing; the vibration measurements of the turbine and pump

were satisfactory and indicated normal operation; oil analysis for the bearings were

acceptable; IST data for the pump indicated no appreciable difference between the

results prior to and after the overhaul of the turbine; outboard bearing temperatures,

while significantly higher than normal, were determined via analysis by a vendor and

concurrence by the turbine manufacturer to stabilize at a temperature that was

acceptable for a 24-hour mission time; analysis demonstrated that adjacent turbine

components would not be affected by the increased bearing temperature; analysis of the

oil at increased temperatures by the oil vendor demonstrated no significant decrease in

oil properties; and the increased bearing temperatures were evaluated by the bearing

manufacturer and determined not to affect the operation of the bearing for a 24-hour

mission time.

Analysis: The inspectors determined the failure to have adequate PMT of the TDAFW

pumps was a performance deficiency and a finding. Using IMC 0612, Power Reactor

Inspection Reports, Appendix B, Issue Screening, dated September 20, 2007, the

inspectors determined that this finding is more than minor because if left uncorrected,

the failure would become a more significant issue.

Using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection

Findings for At-Power Situations, Attachment 1, SDP Phase 1 Screening Worksheet for

IE, MS, and B Cornerstones, dated January 10, 2008, the inspectors determined that

the finding did not result in an actual loss of safety function of a system or train of

equipment. Therefore, the finding is considered to be of very low safety significance

(Green). The inspectors also determined that this finding had a cross-cutting aspect in

the area of human performance because the licensee did not ensure that procedures

were adequate and accurate to assure nuclear safety (H.2(c)).

Enforcement: 10 CFR 50, Appendix B, Criterion V, requires, in part, that activities

affecting quality be prescribed and accomplished by procedures appropriate to the

circumstances. Contrary to this, the licensee failed to prescribe and accomplish

adequate PMT with procedures appropriate to the circumstances to ensure that

after maintenance on safety-related equipment, the equipment returned to service

in an operable condition, an activity affecting quality. Because this finding was of

very low safety significance (Green) and because the finding was entered into the

licensees corrective action program (as CAP 01090456), this violation is being treated

as a Non-Cited Violation (NCV 05000266/2007005-05; NCV 05000301/2007005-05),

consistent with Section VI.A of the NRC Enforcement Policy.

The licensee took immediate corrective actions to address the issue by revising the

appropriate procedures, and at the end of the inspection period the licensee continued to

implement planned corrective actions.

40

Enclosure

.2

Evaluation of Licensees Organizational Response to the 2P-29 TDAFW Pump

Emergent Issue (95003)

b.

Inspection Scope

The inspectors utilized additional inspection hours allowed by IMC 0305 Operating

Reactor Assessment Program, since Point Beach exited Column IV of the NRCs Action

Matrix in 2007, to assess the licensees organizational response to a significant issue

associated with the Unit 2 2P-29 TDAFW pump in November 2007. In particular, the

inspectors focused on the organizational use of human performance tools, the

performance of operations and engineering personnel during the issue, and utilization of

the corrective action program by the organization.

Increased water in the outboard bearing of TDAFW pump 2P-29 was first observed

in June 2007. The licensee performed an operability evaluation at that time and

concluded that the pump was operable because the concentration of the oil was

below the 5,000 pm threshold value for operability established by the licensee, based

on Electric Power Research Institute (EPRI) and vendor guidance. Test results revealed

in June 2007 that the water concentration was approximately 140 ppm and in July

compensatory testing identified an increase to 760 ppm. The licensee continued to

trend increasing water in the oil and developed a contingency plan. On September 21,

the oil sample results revealed water levels had increased to 3,845 ppm, and during the

2P-29 TDAFW pump run, an outboard high temperature alarm occurred. In addition,

operators noted that additional leakage was observed from the turbine outboard gland

area. The licensee commenced implementation of the contingency plan, which included

a pump overhaul.

The overhaul was completed on September 23, and included replacement of the turbine

shaft carbon seal rings and the turbine outboard gland seal casing. The gland and

turbine casings were then sealed with high temperature silicone per the maintenance

procedure. The TDAFW pump was run and oil samples were collected. The water

content was visually estimated at 1,500 ppm, and the licensee concluded that they were

within the bounds of the previous operability evaluation. A second test run conducted

that day revealed less water visually than the first run. Both samples were sent offsite

for analysis. On September 27, the lab results were received, with the first run showing

20,400 ppm of water and the second run showing only 56 ppm of water. Condition

report CAP 01113318 was written; however, the description discounted the higher

sample based on conformational biases of the personnel involved, specifically: high

room humidity; statements from a vendor representative noting that increased leakage

may be expected following overhauls (even though this had never been seen on the

identical turbine for the opposite unit); and high humidity in the room where the samples

were split for offsite analysis. Consequently, CAP 01113318 was closed with no action

taken.

On November 1, 2P-29 was run twice and the water content in the oil was analyzed

at 29,515 ppm for the first run and 17,700 ppm for the second run, supporting the

September 2007 value of 20,400 ppm of water as a valid result. The licensee

subsequently initiated its event response procedure. Revision 2 of operability

Evaluation OPR01098358 was performed and completed on November 3, and required

a compensatory measure of running the turbine and sampling the oil every 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

Over the next several days, the TDAFW pump was run for eight hours, every 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

41

Enclosure

Additional data and responses by the licensee to the inspectors questions necessitated

three additional revisions of the OPR by November 10. On November 13, due to the

continued high water content, the licensee elected to overhaul the turbine. The licensee,

with vendor assistance, identified the following significant as-found conditions during the

overhaul: a gap in the aluminum oil deflector ring attached to the turbine shaft by a set

screw, that provided a direct path for steam to enter the bearing housing along the

turbine shaft; the silicone sealant, particularly around the gland housing and casing,

exhibited a lack of adhesion, also providing a path for steam entering; and the gland

housing, which was replaced in the September 2007 maintenance, was undersized.

Following the November 2007 overhaul, the pump underwent PMT and the outboard

bearing oil samples showed less than 100 ppm of water.

c.

Findings

The inspectors identified three Green findings with associated NCVs as a result of the

inspection activities. Two findings are documented in this Section and a third is

documented in Section 1R15.2 of this report.

b.1

Failure to Take Adequate Corrective Actions to Address Water Ingress Following

Maintenance

Introduction: The inspectors identified a Non-Cited Violation (NCV) of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action, having very low safety significance

(Green) for the licensees failure to take prompt corrective actions to correct the cause of

increased water in the 2P-29 TDAFW pump turbine outboard bearing housing, a

condition adverse to quality, originally identified in September 2007.

Description: On September 24, 2007, following the overhaul of the 2P-29 TDAFW

pump turbine, an oil sample was taken from the outboard bearing housing, following a

four hour run. CAP 01112660 was written, which documented water volume in the oil

sample of 1,000 to 1,500 ppm for the four-hour run. The CAP description concluded that

this was an expected condition. A second shorter pump run was performed, and the

water content in the oil was visually estimated to be 100 ppm. The licensee rationalized

that the initial water content was expected and the CAP was closed with no further

actions taken. Three days later, CAP 01113318 was written and documented that the

outboard oil sample from the first four-hour run was actually 20,040 ppm water, and that

the number was not consistent with the visual indications seen on September 24. The

description in the CAP was presented in a manner which refuted the results based on

conjecture, concluding that the 20,040 ppm results were false readings due to a

laboratory error or an accidental capture of water droplets during the sampling process.

The CAP concluded that, the indicated levels of water in the IT-09A sample are errant.

The CAP was screened by licensee staff and no additional actions were taken to either

characterize the cause of the unexplained increase of water in the oil, or to further

evaluate this unexpected condition identified through testing of the safety-related oil,

following the four-hour TDAFW pump run. The licensee did not consider as a corrective

action, running the pump and obtaining another oil sample to verify that the abnormally

high water content following the overhaul was a false indication.

On November 1, approximately five weeks after the maintenance overhaul, the licensee

ran 2P-29 and sampled the oil. The frequency of running the pump once per month was

established in June 2007, when the moisture in the turbine outboard bearing oil was

42

Enclosure

significantly less than the EPRI and vendor recommended 5,000 ppm. The pump was

run slightly more than two hours and the outboard oil sample drawn revealed 29,515

ppm of water in the oil. After the pump had not run for about eight hours and was then

run for eight hours, 17,700 ppm was found in the outboard bearing oil. The licensee

declared the pump inoperable and revised the original June 2007 operability evaluation.

As described previously, on November 13, the licensee began an overhaul of the

turbine.

The inspectors determined that the original unsatisfactory oil sample results in

September 2007 identified a condition adverse to quality associated with the

safety-related 2P-29 TDAFW pump; however, prompt corrective actions were not taken.

Analysis: The inspectors determined that the licensees failure to implement prompt

corrective actions to address the September 2007 2P-29 TDAFW pump turbine

degraded oil sample results, a condition adverse to quality, was a performance

deficiency and a finding. The inspectors concluded that the finding is more than minor in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, dated September 20, 2007, in that the finding could reasonably be viewed

as a precursor to a significant event. Specifically, the failure to promptly correct the

cause of the oil degradation in a timely manner could result in failure of the TDAFW

turbine.

The significance of this finding was evaluated using IMC 0609, Appendix A,

Determining the Significance of Reactor Inspection Findings for At-Power

Situations, dated January 10, 2008, for the Mitigating Systems Cornerstone. The

risk assessment for the potential loss of safety function is attributed to the performance

deficiencies associated with inadequate maintenance discussed in Section 4OA5.2.b.2

as URI 5000266/2007005-07. This finding, for the failure to implement prompt corrective

actions, did not cause the loss of safety function for greater than the allowed outage

time. The inspectors determined that the finding is of very low safety significance

(Green), because the finding did not involve a design deficiency, there was no actual

loss of safety function, no single train loss of safety function for greater than the TS

allowed outage time, and no risk due to external events. The licensee concluded that

although the pump was initially declared inoperable and the oil was degraded, the

TDAFW pump would have performed its specified safety function. Additionally, the

inspectors determined that the finding had a cross-cutting area aspect in the area of

problem identification and resolution. Specifically, the licensee failed to thoroughly

evaluate the problem with water ingress into the oil, such that a resolution addressed the

cause and extent of condition (P.1(c)).

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in

part, that measures be established to assure that conditions adverse to quality, such as

malfunctions, deficiencies, deviations, defective equipment and nonconformances are

promptly identified and corrected. Contrary to this, a condition adverse to quality,

associated with the turbine of the Unit 2 TDAFW pump 2P-29 was not promptly

corrected following identification in September 2007. Specifically, upon identification of

degraded oil in September 2007, a condition adverse to quality, the licensee did not take

prompt corrective actions. As a result of the failure to take prompt corrective actions, the

pump was declared inoperable until November 2007, following additional oil samples

that revealed the continued degraded condition. Because of the very low safety

significance of this finding and because it was entered into the licensees corrective

43

Enclosure

action program as CAP 01115748, this violation is being treated as an NCV, consistent

with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000301/2007005-06).

The licensee took immediate corrective actions to address the issue, which included

reevaluation of operability and ultimately overhaul of 2P-29, and at the end of the

inspection period the licensee continued to evaluate the causes associated with this

finding.

b.2

Unresolved Item: Failure to Perform Adequate Maintenance Resulting in Increased

Water Ingress

Introduction: The inspectors identified a URI associated with the licensees failure to

perform adequate maintenance on the Unit 2 TDAFW pump turbine in September 2007.

Description: The elevated moisture content in the outboard bearing for the 2P-29 turbine

was present since the last ten-year overhaul was performed in November 2006.

However, while the moisture content levels in the oil from November 2006 until the

September 21, 2007, overhaul were elevated, the levels were below the 5,000 ppm

value documented as acceptable in EPRI and vendor guidance. Steam leakage from

the gland seal or turbine casing joints prior to the September overhaul would not have

been vented away from the bearing housing since the turbine insulation extended over

the top of the gland seal casing and up to the bearing housing. In addition, original

cement-based insulation also blocked the gland seal area vent holes.

The licensee concluded, based on test data, that the 2P-29 turbine overhaul that was

completed on September 23, 2007, significantly increased the moisture content in the

outboard bearing oil. A silicone seal applied at the gland casing to turbine casing joint

failed upon initial service resulting in a steam leak in the area of the outboard bearing

housing. The failure of the sealant could not be attributed to one factor; however, the

licensee did conclude one of the root causes was its maintenance procedures did not

address the special requirements needed when applying sealants, and, therefore, site

personnel did not have adequate instruction or training on the use of sealants. In

addition, the licensee identified that the September 2007 maintenance did not allow for

the proper cure time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for the sealant and exceeded the process time of 30

minutes from when the sealant was applied and the joint was torqued.

In a review of the site maintenance procedures, the licensee also identified an additional

root cause that the site continued to lack adequate guidance on specific assembly

details of the turbine, specifically for the oil deflector ring on the turbine shaft: the

tightening of the oil deflector ring set screw was not discussed; and acceptable

clearances between the turbine shaft and the inner diameter of the oil deflector ring were

not specified.

The licensee identified three additional contributing causes: receipt and installation of a

gland casing from the vendor that had incorrect critical dimensions; previous insulation

work blocked the gland seal vents; and plant personnel did not have adequate guidance

on the installation of insulation. At the end of the inspection period, the licensee

continued to develop and implement corrective actions to address the issues

documented in CAP 01115748.

44

Enclosure

At the conclusion of the inspection, the licensee continued to assess the impact of the

water ingress on the availability of the Unit 2 TDAFW pump to perform its design and

augmented quality functions. There is no current safety concern because the pump was

adequately tested and the current low ingress of water into the bearing housing indicated

that the pumps functionality is currently maintained for all licensing and design basis

events. This issue is an Unresolved Item (URI 05000301/2007005-07) until the NRC

reviews the licensees past availability assessment.

.3

Evaluation of the Licensees Independent Assessment of Engineering (95003)

a.

Inspection Scope

The inspectors utilized additional inspection hours allowed by IMC 0305, since Point

Beach exited Column IV of the NRCs Action Matrix in 2007, to assess the licensees

independent assessment of engineering. The licensee committed as part of its response

to the Confirmatory Action Letter CAL 3-04-001, Revision 1, dated April 14, 2006, to

perform alternating independent and self-assessments of the engineering and corrective

action programs. In July 2007, the licensee performed an independent assessment of

engineering performance. The inspectors reviewed the charter for the assessment,

observed the independent assessment team, reviewed the final report, and reviewed the

proposed corrective actions.

b.

Observations and Assessment

The team consisted of four experienced individuals from other utilities and a consulting

firm. The team assessed licensee engineering performance in five areas: fundamentals

of engineering, equipment reliability, configuration management, corrective actions, and

operating experience. The assessment teams overall conclusions were: engineering

rigor and overall quality has improved and has been sufficient for successful

management of potential challenges to design bases and equipment reliability;

unresolved plant material conditions present substantial ongoing challenges; a plateau

may have been reached for engineering improvement; and additional resources and

continued effort will be required to sustain the improvements that have already been

obtained and to bridge the remaining gaps to engineering excellence.

The assessment team identified the following overall issues for attention: most recent

engineering products are of high quality, but examples of products with less than

adequate rigor are still produced; engineering needs to be more predictable and

accountable with respect to schedules; important longstanding issues were not resolved;

engineering resources may not be adequately matched to engineering obligations; the

preventive maintenance optimization and single point vulnerability projects have

languished and, as a consequence, the station had not benefited from the improved

material condition and safety margins; although a list of low margin issues had been

established, there did not appear to be a quantification of the lost margin associated with

these issues or an evaluation of the cumulative effects; it was not clear that cumulative

effects of conditions adverse to quality were being addressed and the large number of

open conditions presented a challenge to effectiveness of such a review; and the

corrective action process was not used to the full potential, specifically: trending was not

being used as effectively as it could be; more effective use of corrective action

processes for vendor products was warranted; and expectations for a close to fix

solution, versus an apparent cause evaluation warranted examination.

45

Enclosure

The overall recommendations from the assessment team were 1) to maintain highly

visible management commitment to rigor and continue associated empowerment, and

2) to implement the specifically identified corrective actions for issues with predictability,

resolution of longstanding issues, prevent maintenance optimization, cumulative effects

of material condition, more aggressive use of corrective action processes, margin

issues, and engineering resources.

The inspectors confirmed that the licensee had developed plans and corrective actions

to address the issues for attention identified by the Independent Assessment Team.

.4

Evaluation of the Independent Assessment of the Corrective Action Program (95003)

a.

Inspection Scope

The inspectors utilized additional inspection hours allowed by IMC 0305, since Point

Beach exited Column IV of the NRCs Action Matrix in 2007, to assess the licensees

independent assessment of the corrective action program. The licensee committed as

part of its response to the Confirmatory Action Letter CAL 3-04-001, Revision 1, dated

April 14, 2006, to perform alternating independent and self-assessments of the

engineering and corrective action programs. The inspectors reviewed the charter for the

assessment of the corrective action program in August 2007, observed the independent

assessment team, reviewed the final report, and reviewed the proposed corrective

actions.

b.

Observations and Assessment

The team consisted of four experienced individuals from other utilities and a consulting

firm. The team concluded that although measurable improvement in the corrective

action program had been achieved over the last 12 months, several opportunities for

improvement needed to be addressed in order to achieve improved performance. The

team noted the following opportunities for improvement: the effectiveness and quality of

apparent cause evaluations needed to be improved; the number of corrective action

program performance indicators above target with no detailed recovery plan indicated

that timeliness continued to be an issue, corrective action program backlog, in particular,

has been increasing; the ease of CAP initiation via computer (Passport software) and

providing feedback to the CAP initiator for CAPs which are closed by the management

screening committee with no action; trending has not been effective at identifying

adverse trends through the quarterly Department Roll-Up Meetings and Passport issues

continue to impede trending; effectiveness reviews for corrective actions to prevent

recurrence needed to consider effectiveness from a broader perspective; additional

opportunities for improvement were identified in apparent cause evaluations for NRC-

identified findings and on the effectiveness of certain actions specified to correct the

January 2007 corrective action program self-assessment issues.

The independent assessment team concluded that some positive features of the

corrective action program included: management was highly engaged in the program

and the screening committee appears to be highly effective; root cause evaluations were

thorough and comprehensive, and effectiveness review criteria were clearly specified;

format consistency has improved for apparent cause evaluations, effectiveness reviews,

and department roll-up meeting reports; the Performance Assessment Review Board

was involved in reviewing the backlog of open CAPs by department; and most actions

46

Enclosure

taken to address issues from the January 2007 corrective action program self-

assessment had resulted in measurable improvement.

The inspectors confirmed that the licensee had developed plans and corrective actions

to address the opportunities for improvement identified by the Independent Assessment

Team.

.5

(Closed) URI 05000266/2006004-05; 05000301/2006004-05: Inadequate 10 CFR 72.48

Screening to Evaluate Possible Thermal Effects on Fuel Cladding

Introduction: The inspectors identified one violation of 10 CFR 72.48(c)(1) in which the

licensee failed to obtain a Certificate of Compliance (CoC) amendment pursuant to

10 CFR 72.244 for changes made in the spent fuel storage cask operating procedures

during the 2004 loading campaign as described in the FSAR and these changes in the

procedures constituted a change in the terms, conditions, or specifications incorporated

in the CoC. Specifically, although Point Beach changed an operating procedure

described in the FSAR that allowed pump down of water from the dry shielded canister

to occur much earlier in the process; Point Beach failed to identify that the following TS,

which was incorporated in the CoC, would have required changes that needed prior

NRC approval: TS 1.2.17a, 32PT Dry Storage Canister (DSC) Vacuum Drying Duration

Limit.

Description: During the fall 2004 campaign, the licensee used the new NUHOMS 32-PT

cask design and modified the sequence of its loading procedures from the generic

operating procedures stated in Chapter M.8 of the FSAR. The change consisted of

draining all of the water from the canister cavity prior to welding the inner top cover on,

whereas the FSAR prescribed draining some of the water from the canister

(approximately 750 gallons), then welding the top inner cover and then draining the

remainder of the water from the canister. In the 10 CFR 72.48 screening, the licensee

failed to evaluate the effect of the water removal during draining and welding on the fuel

cladding temperature. The inadequate screening failed to identify that TS 1.2.17a,

32 PT DSC Vacuum Drying Duration Limit, which was incorporated in the CoC, would

have required a change that needed prior NRC approval. This amendment to the CoC

would address any affects on the vacuum drying time limits that may result from the

potentially higher fuel cladding temperature. The initial fuel cladding temperature, at the

start of vacuum drying in the procedure that deviated from the FSAR, could be higher

than the FSAR assumed value of 215 °F. An assumed temperature of the fuel cladding

higher than the 215 °F basis in the FSAR may result in a shorter vacuum drying time

than that specified in TS 1.2.17a. The licensee loaded five casks utilizing the different

loading process.

Subsequently, in 2006, the licensees cask vendor, Transnuclear, performed a NUHOMS

32PT drain down evaluation (Calculation No. NU32PT-0420) to address the issues with

the vacuum drying duration limit and fuel cladding temperature. The inspectors

reviewed the calculation, which concluded that the maximum fuel cladding temperature

for the 32PT DSC with a heat load of 16.88 kilowatts (kW) (highest heat load for the

32PT DSC amongst users of this canister at the time) was 720 °F. The 720 °F

temperature was below the allowable limit of 752 °F. Therefore, no time limitation was

necessary for vacuum drying of the 32PT DSC when the total decay heat load was

16.88 kW or below.

47

Enclosure

Transnuclear also performed another evaluation (Calculation NUH32PT-0421) in which it

modeled a loading configuration that resulted in the maximum fuel cladding temperature

for vacuum drying. This loading configuration produced a 22.4 kW total heat load.

TS 1.2.17a stated that the limit for duration of vacuum drying was 31 hours3.587963e-4 days <br />0.00861 hours <br />5.125661e-5 weeks <br />1.17955e-5 months <br /> for a 32PT

DSC with a heat load greater than 8.4 kW and up to 24 kW after initiation of vacuum

drying. This value of 22.4 kW total maximum heat load was within the maximum TS fuel

cladding temperature for the 24 kW heat load. The results of this evaluation justified

using a constant temperature of 215 °F for DSC during handling, welding, and vacuum

drying operations, and indicated that after 31 hours3.587963e-4 days <br />0.00861 hours <br />5.125661e-5 weeks <br />1.17955e-5 months <br /> of vacuum drying the maximum fuel

cladding temperature was 739 °F, below the allowable limit of 752 °F. The maximum

fuel cladding temperature reached the allowable limit of 752 °F at 67 hours7.75463e-4 days <br />0.0186 hours <br />1.107804e-4 weeks <br />2.54935e-5 months <br /> after the start

of the DSC drainage. Thus, the evaluation concluded that the time limit of 31 hours3.587963e-4 days <br />0.00861 hours <br />5.125661e-5 weeks <br />1.17955e-5 months <br /> for

vacuum drying was acceptable.

Analysis: The inspectors determined that the failure to obtain a CoC amendment

pursuant to 10 CFR 72.244 for changes made in the spent fuel storage cask operating

procedures, as described in the FSAR, was a performance deficiency and a finding.

This finding is more than minor because it had the potential to impact the NRCs ability

to perform its regulatory function, since the licensee failed to receive NRC approval for a

change in this licensed activity. A CoC amendment was required since these changes in

the procedures constituted a change in the terms, conditions, or specifications

incorporated into the CoC. The inspectors determined that the finding was not suitable

for SDP evaluation because the noncompliance involved 10 CFR Part 72 dry fuel

storage activities. Therefore, this finding was reviewed by Regional Management and

dispositioned using traditional enforcement.

Enforcement: 10 CFR 72.48(c)(1) states, in part, that a certificate holder may make

changes in the facility or spent fuel storage cask design as described in the FSAR (as

updated), make changes in the procedures as described in the FSAR (as updated),

without obtaining: (a) a Certificate of Compliance (CoC) amendment submitted by the

certificate holder pursuant to 10 CFR 72.244; if: (b) a change in the terms conditions, or

specifications incorporated in the CoC is not required; and (c) the change, test, or

experiment does not meet any of the criteria in paragraph in 10 CFR 72.48(c)(2).

Contrary to this, in an approved 10 CFR 72.48 evaluation, Point Beach failed to obtain a

CoC amendment pursuant to 10 CFR 72.244 for changes made in the spent fuel storage

cask operating procedures as described in the FSAR (as updated) and these changes in

the procedures constituted a change in the terms, conditions, or specifications

incorporated in the CoC. Specifically, although Point Beach changed an operating

procedure described in the FSAR which allowed pump down of water from the dry

shielded canister to occur much earlier in the process; Point Beach failed to identify that

the following TS, which was incorporated in the CoC, would have required changes that

needed prior NRC approval: TS 1.2.17a, 32PT DSC Vacuum Drying Duration Limit.

Because this violation was of very low safety significance, was not repetitive or willful,

and was entered into your corrective action program, this violation is being treated as an

NCV of 10 CFR 72.48(c)(1), consistent with Section VI.A.1 of the NRC Enforcement

Policy (NCV 05000266/2007005-09; 05000301/2007005-09).

The licensee entered the issue into the corrective action program as CAP 01026070 and

implemented corrective actions, including revising the loading procedure to reflect the

sequence described in the FSAR prior to loading the next cask (cask 6).

48

Enclosure

.6

(Closed) URI 07200005/2004003-01: Adequacy of Design Calculation,

PBNP-305336-SO1

During an October through December 2004 NRC inspection, inspectors identified one

URI associated with the adequacy of the licensees auxiliary building structure and the

crane design basis during a seismic event. The licensee received an NCV of

10 CFR 72.122(2)(i), documented in Inspection Report 07200005/2004-003(DNMS),

regarding failure to demonstrate that the crane, a component important to safety, was

designed to withstand the effects of an earthquake without impairing its capability to

perform its intended function. Upon further review, the inspectors identified other

deficiencies in the structural analysis of the building and the crane for which the URI was

opened. There was no response spectra analysis performed on the building to model its

response due to an earthquake at different elevations, such as that of the crane. Also,

the inspectors could not independently verify that the basis for the horizontal

accelerations in all of the calculations used for the auxiliary building and the crane were

adequate. In response to these questions, the licensee constructed a detailed computer

model of the steel portion of the auxiliary building. The preliminary results from an

analysis using this model demonstrated that the original acceleration values were

conservative and adequate to demonstrate compliance with regulations and the ability of

the building and the crane to sustain up to a 125-ton load under an earthquake scenario.

In addition, the licensee hired an independent consultant who confirmed the licensee=s

results. The inspectors were not able to validate these conclusions since the

appropriate documentation was not available at the time of the inspection and a

complete analysis was not completed. However, the licensee committed to perform a

full analysis of the auxiliary building and the crane response under a seismic event with

the current plant conditions.

The licensee performed an analysis of the Class 3 Primary Auxiliary Building (PAB)

Steel Superstructure in Calculation PBNP-305336-SO1, Structural Analysis of Central

PAB with Crane Load of 125 Tons, Revision 1, dated April 3, 2006. During the current

inspection, NRC staff reviewed the calculation results and discussed the assumptions

with licensee personnel. The analysis demonstrated the capability of the structure to

support the crane with a load of 125 tons in case of a seismic event once the welded

connection of the gusset and Columns 10U and 13U were strengthened. Thus, the

calculation verified that the requirements of NUREG-0612 and 10 CFR 72.122(b)(2)(i)

were satisfied. The inspectors concluded that the revised calculation was adequate to

demonstrate compliance with regulations and the ability of the building and the crane to

sustain up to a 125-ton load under an earthquake scenario.

4OA6 MANAGEMENT MEETINGS

.1

Exit Meeting Summary

On January 10, 2008, the inspectors presented the inspection results to Mr. James

McCarthy and other members of the licensee staff. The licensee acknowledged the

issues presented. The inspectors asked the licensee whether any materials examined

during the inspection should be considered proprietary. No proprietary information was

identified.

49

Enclosure

.2

Interim Exit Meeting

An interim exit meeting was conducted for:

Maintenance Effectiveness Periodic Evaluation with Mr. Walt Smith,

Acting Plant Manager on November 2, 2007.

Biennial Licensed Operator Requalification Program Inspection with

Mr. J. McCarthy on November 9, 2007.

Overall assessments of the annual operating test via telephone with

Mr. C. Sizemore on November 21, 2007.

Emergency Preparedness inspection with Ms. Ray and Mr. Tulley on

December 13, 2007.

Occupational radiation safety cornerstone radiation monitoring instrumentation

and protective equipment with Messrs. J. McCarthy and G. Packard and other

licensee staff on December 14, 2007.

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

R. Amundson, General Supervisor Operations Supervisor

C. Butcher, Site Engineering Director

G. Casadonte, Fire Protection Coordinator

W. Godes, Training Supervisor

R. Harrsch, Operations Manager

M. Hayes, Radiation Protection Supervisor

C. Jilek, Site Maintenance Rule Coordinator

J. McCarthy, Site Vice-President

G. Packard, Plant Manager

S. Pfaff, Performance Assessment Supervisor

K. Phillips, Outage Manager

M. Ray, Regulatory Affairs Manager

C. Sizemore, Training Manager

T. Schmitt, Lead health Physics Technician

S. Tulley, Emergency Preparedness Manager

B. Vandervelde, Maintenance Manager

D. Villicana, Radiation Protection General Supervisor

G. Young, Nuclear Oversight Manager

Nuclear Regulatory Commission

M. Kunowski, Chief, Reactor Projects, Branch 5

J. Cushing, Point Beach Project Manager, Office of Nuclear Reactor Regulation

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened and Closed 05000266/2007005-01; 05000301/2007005-01

FIN

Failure to Control Loose Materials Classified as Tornado

Hazards (Section 1R01.1)05000266/2007005-02; 05000301/2007005-02

FIN

Failure to Adequately Assess Operability of Service Water

Pump P-32C (Section 1R15.1)05000301/2007005-03

NCV

Failure to Perform Operability Evaluations for Turbine-Driven

Auxiliary Feedwater Pump 2P-29 (Section 1R15.2)05000266/2007005-04; 05000301/2007005-04

NCV

Failure to Have Adequate Procedures for the Refueling

Water Storage Tank (Section 4OA3.1)05000266/2007005-05; 05000301/2007005-05

NCV

Failure to Perform Adequate Post-Maintenance Testing for

the Turbine-Driven Auxiliary Feedwater Pumps

(Section 4OA5.1)

2

Attachment 05000301/2007005-06

NCV

Failure to Adequately Evaluate a Condition Adverse to

Quality Associated with Turbine-Driven Auxiliary Feedwater

Pump 2P-29 (Section 4OA5.2.b.1)05000266/2007005-08; 05000301/2007005-08

NCV

Failure to Provide Adequate Guidance to Ensure the

Operability of the MS System During a Steam Generator

Tube Rupture. This Item was described in NRC Inspection

Report 2007301, dated August 21, 2007, as Item Numbers05000266/2007301-01 and 05000301/2007301-01; however,

this item is being repeated in this table for NRC Plant Issues

Matrix tracking.05000266/2007005-09; 05000301/2007005-09

NCV

Inadequate 10 CFR 72.48 Screening to Evaluate Possible

Thermal Effects on Fuel Cladding (Section 4OA5.5)

Opened 05000301/2007005-07

URI

September 2007 Maintenance Activities Associated with

Turbine-Driven Auxiliary Feedwater Pump 2P-29

(Section 4OA5.2.b.2)

Closed 05000266/2006011-01; 05000301/2006011-01

VIO

Failure to Update Final Safety Analysis Report with Reactor

Head Drop Analysis and Obtain NRC Approval

(Section 4OA3.2)05000266/2006004-05; 05000301/2006004-05

URI

Inadequate 10 CFR 72.48 Screening to Evaluate Possible

Thermal Effects on Fuel Cladding (Section 4OA5.5)

07200005/2004003-01

URI

Adequacy of Design Calculation, PBNP-305336-SO1

(Section 4OA5.6)

3

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

Issue Reports:

- CAP 01114731; Loose Materials Found in the Protected Area; October 19, 2007

- CAP 01114637; Material in Yard; 10/18/2007

- CAP 01094135; Tornado Hazards Identified Performing PC 99; May 25, 2007

- CAP 01102551; Tornado Hazards Identified Performing PC-99; July 19, 2007

- CAP 01112508; Tornado hazards Identified Performing PC-99; September 21, 2007

- CAP 01098214; 3 or More Tornado Hazards in Single Inspection. Area; June 21, 2007

Procedures:

- PC 99; Tornado Hazards Inspection Checklist; Revision 0

- AOP-13C; Severe Weather Conditions; Revision 17

- NP 1.9.6; Plant Cleanliness and Storage; Revision 22

1R04 Equipment Alignment

- CL 11A G01; G01 Emergency Diesel Generator Checklist; Revision 22

- CL 11A G02; G02 Emergency Diesel Generator Checklist; Revision 26

- CL 13, Part 1; Auxiliary Feedwater Lineup Unit 1 Turbine Driven; Revision 36

- CL 13, Part 1; Auxiliary Feedwater Lineup Unit 2 Turbine Driven; Revision 40

- CL 13, Part 1; Auxiliary Feedwater Lineup Motor Driven; Revision 42

- O-SOP-G01-001; Maintenance Operation for Emergency Diesel Generator G01; Revision 5

- O-SOP-G01-002; Maintenance Operation for Emergency Diesel Generator G02; Revision 8

- O-TS-AFW-002; Auxiliary Feedwater System Valve and Lock Checklist - Monthly; Revision 10

1R05 Fire Protection

Fire Hazards Analysis Report; January 2007 Revision

1R07 Heat Sink Performance

Documents:

- Bio/Silt Fouling Inspection Form for EDG G01 Heat Exchanger; November 2007

- Bio/Silt Fouling Inspection Form for EDG G02 Heat Exchanger; December 2007

1R11 Licensed Operator Requalification Program

Issued Reports:

- Point Beach ROP Plant Issue Matrix from 09/01/2005 to 10/11/2007; October 11, 2007

- Point Beach Nuclear Plant, Units 1 and 2 NRC Integrated Inspection Reports; dated various

from October 26, 2005, through October 26, 2007

4

Attachment

- LER 266/2005-007-00; Control Rod Movement With Refueling Cavity Water Level Below

TS 3.9.6 Limit; January 16, 2006

- Nuclear Oversight Assessment Reports for Point Beach; dated various 2006 and 2007

- Operations Training Advisory Committee Meeting Minutes; dated various from

March 15, 2006, through September 13, 2007

- LOR Curriculum Review Committee Meeting Minutes; dated various from March 7, 2006,

through September 28, 2007

- AO Curriculum Review Committee Meeting Minutes; February 21, 2007

- Completed TRQM 19.32; Activation of an Inactive SRO License; Two Separate Forms;

February 24, 2006, and June 5, 2006

- Completed PBF-2094; NRC License Active Status Tracking; dated various

- Completed PBF-6097; Operations Watchstander Temporary Restriction Form; dated various

- Licensed Operator Quarterly Status Report; dated various

- Operations Continuing Training End of Cycle Reports; dated various 2006 and 2007

- QF-1050-01a; Course/Cycle Feedback Summary Form; dated various 2006 and 2007

- 2007 - 2008 LOR Biennial Training Plan (BTP); Revision 3

- 2006 NRC Biennial Written Exams; dated various

- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Summary

- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Test Item Statistics

- Point Beach Nuclear Plant 2005/2006 Biennial Written Exam Sample Plan

- Evaluation ID# PB-LOR-006-001E; Written Exam Item Review; August 6, 2007

- Management Observations of Training 2006 and 2007

- Licensee 71111.11 Pre-Inspection; August 13, 2007

- LOR Cycle Attendance Sheets; dated various

- Completed QF-1040-04; Remediation Training Form; dated various

- Completed QF-1040-15; Self-Study/Make-Up Training Form; dated various

- Completed QF-1073-01; Walkthrough Exam Summary; Exam Weeks 5 and 6 of 2007; dated

various

- Completed QF-1073-02; Crew Simulator Evaluation Summary; Exam Weeks 5 and 6 of 2007;

dated various

- Completed QF-1073-03; Individual Operator Simulator Examination Summary; Exam Weeks 5

and 6 of 2007; dated various

- Completed QF-1073-04; Remediation Training Form; Exam Weeks 5 and 6 of 2007; dated

various

- Simulator Review Committee Meeting Minutes; dated various from March 2, 2006, through

September 13, 2007

- FP-T-SAT-81; Simulator Testing and Documentation; Revision 4

- SWO 05-0039; Rehost Simulator PPCS, March 22, 2005

- SIMGL C1.4; Install and Test U1C31; November 2, 2007

- SIMGL C3.3; Simulator Certification Testing; September 21, 2005

- SCT 6.8.37.5; Stuck Open Condenser Dump Valve; August 29, 2006

- SCT 6.3.2; 75 Percent Power Heat Balance; July 12, 2006

- SCT 6.1.4; 100 Percent Steady State Drift Test; July 11, 2006

- SCT 6.8.13.3; Loss of a 4160 Volt Bus; December 7, 2006

- SCT 6.8.16.3; Generator Inadvertent Trip; July 18, 2006

- SCT 6.5.1; Manual Reactor Trip; April 3, 2006

- SCT 6.5.8; Loss of Coolant Accident With Loss of Offsite Power; March 30, 2006

- Simulator Review Committee Meeting Minutes; June 28, 2007

- Simulator Review Committee Meeting Minutes; February 12, 2007

- Simulator Work Orders Closed Out in Previous 12 Months; November 1, 2007

- List of Open Simulator SWOs; November 1, 2007

5

Attachment

- FP-T-SAT-80; Simulator Configuration Management; September 28, 2007

- FP-T-SAT-81; Simulator Testing and Documentation; September 28, 2007

- SIMGL C3.3; Simulator Certification Testing; September 21, 2005

- SIMGL C1.4; Simulator Modifications and Core Load Changes (Completed for Unit 1);

November 2, 2007

- ANSI/ANS-3.5-1985; Nuclear Power Plant Simulators for Use in Operator Training;

October 25, 1985

- Regulatory Guide 1.149; Nuclear Power Plant Simulation Facilities for Use in Operator License

Examinations; Revision 1; April 1987

- ANSI/ANS-3.4-1996; Medical Certification and Monitoring of Personnel Requiring Operator

Licenses for Nuclear Power Plants; February 7, 1996

- Regulatory Guide 1.134; Medical Evaluation of Licensed Personnel for Nuclear Power Plants;

Revision 3; March 1998

- Seven Licensed Operators Medical Records; dated various

- TRR 01116172; Review Two Exam Bank Questions for Difficulty Level Changes;

November 8, 2007

- TRR 01116174; Review Two JPMs for Difficulty Level; November 8, 2007

Procedures:

- FP-T-SAT-73; Licensed Operator Requalification Program Examinations; Revision 2

- JPM P000.042bAOT; Lineup for Transfer to Containment Sump Post-Accident Recirculation;

Revision 4

- SEG # PB-LOR-07E-001S; High Impact Session - PZR Pressure Transmitter RTS,

EH Malfunction and Containment Sump Recirculation; Revision 0

- EOP-1.3 Unit 1; Transfer to Containment Sump Recirculation - Low Head Injection;

Revision 39

- FL-LOR-TPD; NMC Fleet Licensed Operator Requalification Training Program Description;

Revision 0

- TRPR 33.0; Training Program Description; Licensed Operator Requalification Training

Program; Revision 25

- OM 3.10; Operations Personnel Assignments and Scheduling; Revision 23; August 9, 2007

- FP-T-SAT-71; NRC Examination Security Requirements; Revision 0

- CAP 01040650; Simulator PPCS Failed Completely, Affecting LOR As Found; July 20, 2006

- CAP 01073895; EP Issues from LOR 2006 Annual Operating Exams; January 25, 2007

- CAP 01092718; LOR Cycle 07C Schedule Affected by Simulator Malfunctions; May 15, 2007

- CAP 01111841; RWST Temp Found High OOS on Logs; September 18, 2007

- CAP 01113938; Operations Quarterly Status Report Accuracy Questioned; October 9, 2007

- CAP 01115710; Annual Operating Exam Security Lapse Results in Rework;

November 1, 2007

- NP 1.10.1; Record Keeping for NRC Licensed Operators; July 20, 2005

- OM 4.3.2; EOP/AOP Verification/Validation Process; Revision 15; October 29, 2007

CAPs/PCRs/TRRs Initiated for NRC-Identified Issues:

- CAP 01115978; Watchstander Restriction Form Not Filled Out Correctly; November 7, 2007

- CAP 01116144; PCRs Generated from CDBI Closed Out With No Action Taken;

November 8, 2007

- CAP 01116160; Simulator PPCS Problems During Exams; November 8, 2007

- PCR 01116095; Revise EOP 1.3 Unit 1; November 8, 2007

- PCR 01116097; Revise EOP 1.3 Unit 2; November 8, 2007

6

Attachment

1R13 Maintenance Risk Assessments and Emergent Work Control

- NP 10.3.6; Shutdown Safety Review and Safety Assessment; Revision 19

- Safety Monitor Calculation Reports for Units 1 and 2 for Applicable Work Weeks

- Work Week Execution Schedules for the Applicable Work Weeks

- Operator Logs for the Applicable Work Weeks

1R15 Operability Evaluations

Issue Reports:

- CAP 01111251; Discrepancy in CAF BHP Measured vs. Vendor Data; September 13, 2007

- OPR 154; Overload Concerns of Safeguards 480V AC Load Control and Motor Control

Centers; Revisions 1 Through 3

- OPR 157; EDG Operability Related to Electrical Loading During Certain Accident Scenarios;

Revision 3

- AR 01106938-01; Past Operability of P-32C; 10/25/2007

- CAP 01098680; P-32C SW Pump Vibration Nearing Acceptance Criteria Limit; June 24, 2007

- OPR 01098680; P-32C, Service Water Pump; Revision 0

- ACE 01098680-02; P-32C Vibration Issues; October 5, 2007

- CAP 01105929; P-32C SW Pump Fails IT-07C Testing; August 8, 2007

- CAP 01114171; OI 35C Requires Extensive Rewriting; October 11, 2007

- CAP 01119241; Concerns of PBNPs Use of IST Trend Data in OPRs; January 4, 2008

- CAP 01112660, 2P-29 Outboard Bearing Water Following IT-09A; September 24, 2007

- CAP 01113318, IT-09A Oil Analysis Results Not As Expected for 2P-29; September 27, 2007

- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 2,

November 3, 2007

- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 3,

November 4, 2007

- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 4,

November 7, 2007

- OPR1098358, Moisture Observed in Oil Sample From 2P-29 Outboard Bearing, Revision 5,

November 10, 2007

Procedures:

- OI-35C; 480V Electrical Load Conservation; Revisions 3 and 4

- IT-07C; P-32C Service Water Pump (Quarterly); Revision 18

1R17 Permanent Plant Modifications

- Engineering Modification 05-006 and Engineering Changes EC1590 and 1591 Associated

With the Replacement of the EDG Heat Exchangers for EDGs G01 and G02

1R19 Post-Maintenance Testing

Procedures:

- RMP 9216-5;Service Water Pump Bowl Assembly Inspection and Maintenance; Revision 3

- IT 07E; P-32E Service Water Pump (Quarterly); Revision 19

- RMP 9387; AC Induction Motor MCE Testing Procedure; Revision 4

- IT-21; Charging Pumps and Valves Quarterly; Revision 18

- RMP 9003-1; Charging Pump Overhaul; Revision 6

7

Attachment

Work Orders:

- WO 302859-01; Service Water Pump Maintenance; October 24, 2007

- WO 300182-02; P-32E Service Water Pump Lower Than Expected Insul Resistance Reading;

October 24, 2007

- WO 219880; CVCS Charging Pump Modification - Pump 1P2B Renovation; Revision 0

1R22 Surveillance Testing

Procedures:

- IT-65; Containment Isolation Valves Quarterly; Revision 35

- PBTP 158; Leak rate Testing of 2SC-966C Containment Isolation Valve at Power; Revision 0

- IT-09A; Cold Start of the Turbine Driven Auxiliary Feedwater Pump Unit 2; Revision 45

- TS-81; Emergency Diesel Generator G01; Revision 75

- TS-82; Emergency Diesel Generator G02; Revision 76

1R23 Temporary Plant Modifications

Engineering Change:

- EC11633; Furmanite Injection of 2MS-232A MSR Valve

Work Orders:

- WO 340064; Furmanite Injection of 2MS-232A MSR Valve

- WO 346804; Furmanite Injection of 2MS-232A MSR Valve

2OS3 Radiation Monitoring Instrumentation and Protective Equipment

Issue Reports:

- Point Beach Nuclear Plant Radiation Monitoring System Health Report; December 6, 2007

- Snapshot Self-Assessment Report; SCBA Maintenance and User Training;

November 30, 2007

- Snapshot Self-Assessment Report; IP 71121.03 Inspection; November 30, 2007

- Snapshot Self-Assessment Report; 2006 INPO Area for Improvement - Radiation Monitoring

Instrument Program; November 23, 2007

- Radiation Protection Instrument Inventory and Calibration Due Date Report;

December 7, 2007

- Radcal Corporation Certificate of Conformance for Electrometer/Ion Chamber Model 20-X5-

1800 (SN 21707), Model 20X5-3 (SN 21548) and Model 20-X5-60 (SN 21344);

September 21, 2005

- Report of Calibration for the Canberra Fastscan Whole Body Count System at the Point Beach

Nuclear Plant; January 26, 2007

- Report of Evaluation of Isotopic Mixture and RP Programs; January 31, 2007

- Calibration Record for MGP Instrument Model AMP-100 (SN 474103); March 24, 2007

- Calibration Record for Eberline Instrument Model AMS-4 (SN A021); January 27, 2007

- Point Beach Emergency Plan Manual; EP 7.0 - Emergency Facilities and Equipment;

Revision 51

- Qualification Matrix and Training Status for Respiratory Protection; December 11, 2007

- Lesson Plan No. PB-SHE-004-SCRL; Respiratory Protection; Revision 1

- Scott Posicheck 3; Visual and Functional Test Records for Point Beach SCBA Units;

March 20, 2007

8

Attachment

Procedures:

- HPIP 7.52.4; PM-7 Personnel Monitor Checks; Revision 12

- HPIP 7.52.1; Personnel Contamination Monitor (PCM-1B/1C) Source Response Check;

Revision 13

- HPIP 5.66; Functional Check of the Gamma-60 Portal Monitor; Revision 21

- HPIP 2.1.1; Response Checks of Portable Survey Instruments; Revision 9

- HPIP 1.74; Operation of the Canberra Whole Body Counter; Revision 7

- HPCAL 3.2; Area Monitor Calibration Procedure DA1-1 and DA1-6 Detector Assemblies and

Associated Calibration Records for Unit 1 and Unit 2 Charging Pump Room (Low Range)

ARMs; December 19, 2006, and September 15, 2006

- HPCAL 3.3; Area Monitor Calibration Procedure DA1-4 and DA1-5 Detector Assemblies and

Associated Calibration Records for Unit 1 and Unit 2 Charging Pump Room (High Range)

ARMs; February 15, 2007, and February 12, 2007

- HPCAL 3.2 Calibration Record for Unit 1 and Unit 2 Seal Table ARMs; April 1, 2007, and

October 15, 2006

- HPCAL 3.2 Calibration Record for Unit 1 and Unit 2 Post Accident Sample Line Monitors;

August 13, 2007, and April 17, 2007

- HP CAL 3.2 Calibration Record for Safety Injection Pump Room Low Range and High Range

ARMs; September 18, 2006, and July 17, 2006

- 2ICP 13.017; Containment High Range Radiation Monitoring System Channels 2RE126,

2RE127, 2RE128 Calibration; December 12, 2006

- 1ICP 13.017; Containment High Range Radiation Monitoring System Channels 1RE126,

1RE127, 1RE-128 Calibration; March 14, 2007

- HPCAL 3.11; Containment High Range Detector Response Check Surveillance Record, Unit 1

Detectors (1RE126, 127 and 128), April 11, 2007; and Unit 2 Detectors (2RE126, 127 and

128), October 16, 2006

- HPCAL 1.10.2; Verification of J.L. Shepherd Model 89 Calibrator Dose Rates (Revision 1) and

Associated Output Verification for Calibrator No. 8269 and No. 8228; September 28, 2006

- HPCAL 1.1; Portable Survey Instrument Calibration, Repair and Response Checks;

Revision 18

- NMC Fleet Procedure FP-RP-ICC-01; Instrument Control and Calibration/Functional Testing

Frequencies of RP Instruments; Revision 3

- HPCAL 1.38; Calibration of the Portable Neutron Survey Instrument Analog Smart Portable

(ASP-1), and Associated Calibration Record (Instrument No. 9459); March 9, 2007

- HPCAL 2.8; Eberline PCM-1B Personnel Contamination Monitor Calibration Procedure and

Associated Calibration Record for Monitor No. 7737, October 17, 2007; No.7738,

March 30, 2007; and No. 7739, May 8, 2007

- HPCAL 2.8.1; Personnel Contamination Monitor Detector Efficiency Determination and

Associated Record for Monitor No. 7739; July 13, 2007

- HPCAL 2.11.1; Calibration of the Gamma-60 Portal Monitor and Associated Calibration

Record for Monitor No. 9485, March 12, 2007; and No. 9486, February 22, 2007

- HPCAL 2.21; Calibration of the Eberline Personnel Monitor PM-7 and Associated Calibration

Record for Monitor No. A112 (November 28, 2007); No. A113 (October 29, 2007); and

No. A114; (September 21, 2007)

- HPCAL 2.15; Small Articles Monitor Type SAM 9/11 Calibration and Efficiency and Associated

Calibration Record for Monitor No. 2; September 26, 2007

- PC 75 Part 1; Monthly and Turnaround Maintenance for the Scott Model 4.5 Self-Contained

Breathing Apparatus and Associated Surveillance Records for January 2006 through

December 2007

-

9

Attachment

- PBF-4077(c); Self-Contained Breathing Apparatus Inspection and Maintenance Records for

2006 and 2007

- HPIP 4.51.4; Scott Self-Contained Breathing Apparatus; Revision 8

Work Orders:

- CAP 01048997; Compliance with Fleet Procedure; September 8, 2006

- CAP 01080787; Gamma-60 Source Check Concerns; March 6, 2007

- CAP 00906738; RP Survey Instrument Response Checks and Instrument Sign-Out;

February 7, 2006

- CAP 01081898; Failure of Meter Movement for C-59 Area Monitor RE-111; March 13, 2007

- CAP 01091161; Lack of Bases for RP Equipment Functional Check; May 5, 2007

- CAP 01087730; Possible Trend With Poor Teletector Performance; April 14, 2007

4OA1 Performance Indicator Verification

Issue Reports:

- Monthly Data Elements for RETS/ODCM Radiological Effluents; December 2006 -

November 2007

- Liquid and Gaseous Effluent Summary Data and Dose Calculation Results; March 2007

4OA2 Problem Identification and Resolution

Procedures:

- NP 2.1.4 Operator Burdens; Revision 7

4OA3 Followup of Events and Notices of Enforcement Discretion

Issue Reports:

- CAP 01111841; RWST Temp Found High OOS on Logs; September 18, 2007

- RCE 01111841-01; Unit 2 Refueling Water Storage Tank Temperature High Resulting in

Unplanned TSAC; Revision 1

- RCE 01090456-01; 1P-29 Turbine Driven Auxiliary Feedwater Pump Outboard Bearing Issues

4OA5 Other Activities

Documents:

- EPRI Terry Turbine Guide; Terry Turbine Maintenance Guide, AFW Application TR-1007461

- VTM 0004 Manual: Terry Steam Turbine Company; Auxiliary Feedwater Pump Turbine Drive;

Revision 30

- Technical Data Sheet; Loctite High Temp Red

- Technical Data Sheet; Turbo 50

- Technical Data Sheet; Temp Tite II String Kit

- RCE 01090456-01; IP-29 Turbine Driven Auxiliary Feedwater Pump Outboard Turbine Bearing

Issues

- MPR Report; Point Beach Nuclear Station; Water Containment of AFW Turbine Lube Oil

- Memo on OST Device Drain Plug - Justification of Drain Plug Removal

- Station Logs - From Present Back to June 21, 2007; Focus on Auxiliary Feed Runs

- OCC Logs - November 2006 Outage, September 2007 Overhaul, and November 2007

Overhaul

- 2P-29 Event Folders

- Applicable Oil Analysis Results Record

10

Attachment

- RCE 96-08; Unit 1 Reactor Taken Critical with Both 1P-29 Turbine-Driven Auxiliary Feedwater

Pump Discharge Motor-Operated Valves (1AF-4000, 1AF-4001) Found Shut

- RCE 98-150; Unit 1 Turbine-Driven Auxiliary Feed Pump Turbine Maintenance Rework

- RCE 01115748; 2P-29 AFW Pump Moisture in Oil

Procedures:

- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul

- IT-09A; Cold Start of Turbine-Driven Auxiliary Feed Pump and Valve Test

- OI-62B; Turbine-Driven Auxiliary Feedwater System

Condition Reports and Work Orders:

- CAP 01049806; 1P-29 AFW Pump S/D Due to Low Oil Level in Bubbler; September 12, 2006

- CAP 01051133; Oil Level Problems Encountered During PMT for 1P-29 AFP;

September 19, 2006

- CAP 01062958; Reinstallation of Insulation for 2P-29 TDAFW Pump not Done;

November 20, 2006

- CAP 01068606; 1P-29 Aux Feed Pump Suction Sodium Lab Analysis was High;

December 20, 2006

- CAP 01086108; Additional Paint Removal Required - Not correctly Identified; April 5, 2007

- CAP 01097185; Differences Noted Between RMP 9044-1 and EPRI Guide; June 17, 2007

- CAP 01097732; Improvement Recommendations for RMP 9044-1; June 20, 2007

- CAP 01097736; Declining Trend in 2P-29 TDAFW Pump Speed Noted; June 20, 2007

- CAP 01098358; Moisture Observed in Oil Sample from 2P-29 Turbine Reservoir;

June 21, 2007

- CAP 01098364; AFW Steam Pipe Supports Lubra-Plates Have Been Painted; June 22, 2007

- CAP 01098445; Benchmark in Service Testing of Aux Feed Systems; June 22, 2007

- CAP 01098525; Unit 1 and 2 TDAFW Pump Oil Sampling; June 22, 2007

- CAP 01098536; No Specific Training for Turbine Driven AFPs; June 22, 2007

- CAP 01098615; U2R28 P-29-T: GL 89-13 HX PM Not Properly Documented; June 22, 2007

- CAP 01098626; AFW Casing Sealant Review; June 23, 2007

- CAP 01098633; 1P-29 TDAFW Pump Sentinel Valve Opened on Start; June 23, 2007

- CAP 01099142; Unable to Analyze Water Content of Oil Sample; June 26, 2007

- CAP 01099272; Oil Sample for 2P-29-T May Not Have Been Taken Correctly; June 26, 2007

- CAP 01099402; 2007 AFW Inspection - Review of Additional Engineer Programs;

June 27, 2007

- CAP 01099576; 2P-29 TDAFWP Oil Sample High Water Content; June 28, 2007

- CAP 01099876; Water Content Analysis Results for 2P-29-T OB Bearing; June 29, 2007

- CAP 01100698; IT-08A/IT-09A Do Not Contain 1996 Reg Commitments; July 7, 2007

- CAP 01100865; 1P-29-T Coupling Stretch Not Verified After Re-alignment; July 9, 2007

- CAP 01100874; RMP 9044-1 Contains Vague Guidance for Thomas Coupling Setting;

July 9, 2007

- CAP 01101114; Potential Preconditioning of 1(2)P-29 TDAFW Pump; July 11, 2007

- CAP 01101562; 2P-29 Oil Sample Put on HOLD by Supply Chain Buyer; July 12, 2007

- CAP 01102282; 1P-29 Terry AFP Thomas Coupling Setting Concerns; July 18, 2007

- CAP 01102417; RMP 9044-1, Revision 12, Provides Incorrect Acceptance Criteria;

July 19, 2007

- CAP 01102492; Quarantine Oil Samples Taken from 2P-29-T Under WO 335172;

July 19, 2007

- CAP 01102642; 2P-029-T Oil Dripping from Outboard Bearing Housing Seal; July 19, 2007

- CAP 01102655; Water Still Indicated in Oil from 2P-29-T OB BRG; July 20, 2007

11

Attachment

- CAP 01102868; Higher Than Expected Water in 2P-29-T OB BRG Post Run Sample;

July 21, 2007

- CAP 01102875; 2P-29 Appendix R Functionality; July 21, 2007

- CAP 01102902; Documentation of Observation, 2P-29-T Temperature Indication;

July 22, 2007

- CAP 01102903; Verified Steam Leak at Seal on 2P-29-T OB Bearing; July 22, 2007

- CAP 01103469; Form for Bearing Stabilization on 1P-29 and 2P-29 Is Not Formalized;

July 25, 2007

- CAP 01103520; Potential Improper Oil Issued for 2P-29 Aux Feed Pump; July 25, 2007

- CAP 01103623; Question Concerning Bearing Coolers on P-029 Turbines; July 26, 2007

- CAP 01103841; 1P-29T and 2P-29T OB Steam Gland Drain Lined Pitch Is Incorrect;

July 27, 2007

- CAP 01106373; Evaluate Use of New Governor Drive Coupling on P-29T; August 10, 2007

- CAP 01107473; Oil Storage Requirements Questioned; August 17, 2007

- CAP 01108275; AFP Bearings Failed Vendor Dimensional Inspection; August 23, 2007

- CAP 01108351; 2P-29-T Outboard Bearing Aluminum Fill Plug; August 23, 2007

- CAP 01108355; 1P-29-T Oil Analysis Results Indicated As Alarm; August 23, 2007

- CAP 01108426; 2P-29-T Governor Oil Level High; August 23, 2007

- CAP 01108429; Unexpected Oil Leak Rate While Running 2P-29-T; August 23, 2007

- CAP 01108576; FPL AFW System Focused Assessment - Operations Observations;

August 24, 2007

- CAP 01109045; Oil Analysis Results Questioned; August 28, 2007

- CAP 01109571; P-29-T Inbound Bearing Oiler Upper Casting Slightly Damaged;

August 31, 2007

- CAP 01109572; 2P-29-T Oiler Height Settings; August 31, 2007

- CAP 01112474; 2P-29 Pump Outboard Packing Has Excessive Leakage; September 21, 2007

- CAP 01112475; 2P-29 Outboard Turbine Bearing High Temp Alarm During IT-9A;

September 21, 2007

- CAP 01112533; 2P-29-T Changing Oil and Stabilization; September 21, 2007

- CAP 01112567; Terry Turbine Gland Case leak Off Lines Not Optimal; September 22, 2007

- CAP 01112579; Wrong Revision of Procedure Used for 2P-29-T Work; September 22, 2007

- CAP 01112587; 2P-29-T TDAF Wheel Lap Measurement; September 22, 2007

- CAP 01112596; September 21, 2007 2P-29 Oil Analysis Results; September 22, 2007

- CAP 01112597; 2P-29-T Outboard Terry Turbine Bearing; September 22, 2007

- CAP 01112609; 2P-29-T Outboard BRG Thermocouple Damaged During BRG Crush;

September 23, 2007

- CAP 01112626; 2P-29-T Outboard Bearing Oil Ring Contacting Oil Cooler;

September 23, 2007

- CAP 01112631; 2P-29-T Terry Turbine Casing Bolts; September 23, 2007

- CAP 01112641; RMP 9044-1 Did Not Have Correct torque Value; September 23, 2007

- CAP 01112660; 2P-29-T OB BRG Water Following IT-09A; September 24, 2007

- CAP 01113029; RMP 9044-1 Wrong Revision Used for 2P-29-T Work; September 25, 2007

- CAP 01113318; IT-09A Oil Analysis Results Not As Expected for 2P-29-T;

September 27, 2007

- CAP 01113438; P-29-T Oil Cooler Differences Outboard End; October 1, 2007

- CAP 01113972; IT-290B and IT-295B Makes Reference to Replaced ERPI Guide;

October 10, 2007

- CAP 01113973; Differences Between EPRI Guide and IT-08A, B and IT-09A,B;

October 10, 2007

- CAP 01113978; EPRI Terry Turbine Manual Recommendation for AF; October 10, 2007

- CAP 01115697; 2P-29 TDAFP Inbound Pump Bearing Oil Leak; November 1, 2007

12

Attachment

- CAP 01115748; 2P-29 Moisture in Oil Concern; November 1, 2007

- CAP 01115768; Visual Indications Post IR-09A on November 2, 2007 for Oil;

November 2, 2007

- CAP 01115778; Oil Sampling Concerns for 2P-29 AFW Pump; November 2, 2007

- CAP 01115808; Oil Analysis Results for 2P-29-T on November 3, 2007; November 3, 2007

- CAP 01115810; 2P-29 Returned to OPS in an Operable But Degraded Condition;

November 3, 2007

- CAP 01115819; November 2, 2007 Log Entry for 2P-29 Availability Incomplete;

November 4, 2007

- CAP 01115832; Appears Samples Not Taken Per Request; November 5, 2007

- CAP 01115952; Oil Analysis Results for 2P-29-T from November 5, 2007; November 6, 2007

- CAP 01116158; 2P-29 Governor Gear Drive Oil Color; November 8, 2007

- WO 219237; Uncouple 2P-29 Per Callup Text; March 8, 2006

- WO 219238; Inspect Inboard and Outboard Bearing; March 8, 2006

- WO 219239; Emergency Governor Inspection; March 8, 2006

- WO 219240; Sample Oil in 2P-29 Turbine Governor; March 8, 2006

- WO 219448; Perform Overhaul; October 24, 2006

- WO 267802; ten-Year Overhaul; November 12, 2006

- WO 268232; Sample Oil in 2P-29 Turbine Governor; November 12, 2006

- WO 268233; GL 89-13 - Inspect Bearing Oil Coolers; November 12, 2006

- WO 268234; Emergency Governor Inspection; November 12, 2006

- WO 268235; Uncouple 2P-29 Pump from Its Turbine; November 12, 2006

- WO 334308 Auxiliary Feedwater Pump Terry Turbine Overhaul; September 12, 2007

- WO 334597; Sample and Change Oil as Required; November 9, 2007

- WO 335167; Sample and Change Oil As Required; June 28, 2007

- WO 346758; Auxiliary Feedwater Pump Terry Turbine Overhaul; November 2, 2007

NRC-Identified Condition Reports

- AR 01100068; Closeout Based on Incorrect Info

- AR 01100293; Benchmarking/Snapshot Evaluation for VTI

- AR 01100509; Potential HU Crosscut

- AR 01100985; Cable ZA1327FA Not Included in App

- AR 01101029; Error Noted on Drawing WEST 499B466

- AR 01101383; Near Miss During ILT NRC Exam

- AR 01101421; Untimely Corrective Actions

- AR 01101444; Compliance With Appendix R,Section III

- AR 01101461; Potential Coincident Fire Induced Failure

- AR 01101506; NFPA 13 Issues With G-01 and G-02 R

- AR 01101596; Procedure EOP-3 Change Needed for Bistable Tube Rupture

- AR 01101667; Inconsistent/Inadequate Direction

- AR 01101704; Procedure EOP-3 Steps Out of Sequence

- AR 01102113; Scaffold Clearance Questioned

- AR 01102590; Incorrect Description of Pushbutton

- AR 01103769; Error in Calculation S-11165-035-SW

- AR 01105181; Fire Extinguishers Removed for Annu

- AR 01105290; Inappropriate Screened AR 11033415

- AR 01105804; PI Indicator Does Not Match INPO CD

- AR 01105948; PI-2849 Discharge Pressure on E SW

- AR 01105993; Quench Curve Check Performed

- AR 01106042; Fluctuations Seen on P-32E SW Pump

13

Attachment

- AR 01106118; Façade Groundwater Samples Not Shipped

- AR 01107098; Missing Bolts on Subsoil Drainage

- AR 01107355; Stalling of MOVs while Load Sequencing

- AR 01107452; Lube oil Tank Rupture

- AR 01107461; NRC RP Inspection: Groundwater

- AR 01107485; Weakness Identified in 10 CFR 50.75(g)

- AR 01107520; Debris in Subsoil Drainage System

- AR 01107630; Create Engineering Documents for Flooding

- AR 01107634; Formally Verify Function and Capacity

- AR 01108334; Radiodine Results High - Evaluate

- AR 01108724; Supplement Needed for LAR 249

- AR 01109665; LAR 247 submittal Being Withdrawn

- AR 01109968; 2007 Mid-Cycle Performance Review

- AR 01109992; 2007 EP Drill

- AR 01111043; LER 2007-003 Related AR Severity

- AR 01111296; RCE-01075472 Not Revised per PARB

- AR 01112896; Improvements in Posting and Access

- AR 01112924; Postings in RCA Yard Found Faded

- AR 01112934; Cleanliness in the Drumming Room

- AR 01112981; Point Beach Nuclear Plant Flood Watch Commitment Information

- AR 01113207; NRC Radwaste Inspection/ATCOR Equip

- AR 01113226; NRC Question on 10 CFR 20, Appendix G, A.3

- AR 01113277; Material Condition

- AR 01113347; NRC Radwaste Inspection Request

- AR 01113420; NRC Inspection Debrief

- AR 01113508; Security Documentation Enhancement

- AR 01113563; Security Weapons Documentation

- AR 01114426; Procedure Noncompliance of NP 8.4.1

- AR 01114599; PC 99 May Need To Be Implemented

- AR 01114637; Material in Yard

- AR 01114731; Loose Materials Found in the Protected Area

- AR 01115102; Weakness Identified in Crew Information

- AR 01115108; Unit 2 MFRV Turnover Less Than Complete

- AR 01115189; Scaffold Material in Contact

- AR 01115311; Small Coolant Leak on G-04 EDG

- AR 01115486; Point Beach Nuclear Plant Use of Maintenance Run

- AR 01115556; Requirements of NP 7.7.5 for Maintenance

- AR 01115620; Error Found by Review of Maintenance

- AR 01115703; OPR 01114308 Requires Revision

- AR 01115713; Number of Maintenance Rule Functional Failures

- AR 01115729; Documentation of D-06 Performance

- AR 01115818; Potential SSD Equipment Missing From Documentation

- AR 01115819; November 2, 2007 Log Entry for 2P-29

- AR 01115820; LAR 256, ILRT Interval Extension

- AR 01115838; Revision 3 Required for OPR 1098358

- AR 01115876; EPRI Guidance Not Included in RMP 9

- AR 01115881; Wording in OPR 1098358 May Be Misleading

- AR 01115951; Unit 2 TDAFWP Event - NRC Question

- AR 01115978; Watchstander Restriction Form Not Filed

- AR 01116011; 2P-29 Oil Samples

- AR 01116150; Discrepancy in TAN Values

14

Attachment

- AR 01116158; 2P-29 Governor Gear Drive Oil Color

- AR 01116250; Lack of Sample Splitting Procedure

- AR 01116334; Minor Shaft Pitting - 2P-29

- AR 01116442; 2P-029-T Oil Dregs

- AR 01116533; LAR 256 ILRT Extension Request

- AR 01116589; MSPI Records Missing From EDMS

- AR 01116594; HPIT - Confirmation Bias in Engineering

- AR 01116619; 2P-29-T - OPR Testing Methodology

- AR 01116647; Procedural Temporary Change Chart

- AR 01116658; General Observations Regarding 2P-0

- AR 01116673; Clarification Needed for Sealant

- AR 01116688; Review/Revise OPR 1098358

- AR 01116794; Minor Error Found in CDE

- AR 01116819; Unavailability Guidance for MR and NEI

- AR 01117062; 1RMP-9096 and SLP 2 Revisions Required

- AR 01117126; Revise/Correct EOP Setpoint for L.25 and L.4

- AR 01117152; Revise IP-29 Root Cause to Address Issue

- AR 01117163; MI 32.9 Scaffold Stabilization Criteria

- AR 01117170; Rubber Pads Not Installed on RCP

- AR 01117200; NRC Noted Service Water Drawing - Verification Temperature Indicator

- AR 01117205; NRC Noted Auxiliary Feedwater Drawing

- AR 01117350; IT 40/45 Do Not Contain Caution Statements

- AR 01117459; Façade Wells - H-3 in Ground Water

- AR 01117637; Errors in Calculations - PCI-5344-S02

- AR 01117860; Provide Preliminary Technical Basis - Temporary Storage Items

- AR 01118002; Errors in Calculations - PCI-5344-S01

- AR 01118105; ACE 10434692 - Actions Not Identified

- AR 01118106; PM-7 Functional Check Periodicity

- AR 01118107; H3 Sample Results

- AR 01118141; License Amendment Quality/Timeliness

- AR 01118144; Errors in Structural Calculation

- AR 01118148; Rigging Evaluation Documentation

- AR 01118185; Evaluate Load Handling Procedure

- AR 01118189; NRC BL 2007-01, Security Officer

- AR 01118194; Recommended Improvement to DG-M10

- AR 01118195; SCBA LP Does Not Show How to Change

- AR 01118200; Support Model in Calculation PBNP-9

- AR 01118202; Low Design Margin for Plant Component

- AR 01118207; SCBA Monthly Location Inspection

- AR 01118213; Consider Completing and Audit on SC

- AR 01118259; NRC Inspection Observation

- AR 01118722; NRC Concern About Secondary Sample

- AR 01118844; Clarification Regarding Operability - Implement Recommendations

- AR 01118847; NRC Submittal Rejected

15

Attachment

LIST OF ACRONYMS USED

AC

Alternating Current

ACE

Apparent Cause Evaluation

AFW

Auxiliary Feedwater

AOP

Abnormal Operating Procedure

ARM

Area Radiation Monitor

ASME

American Society of Mechanical Engineers

CAP

Corrective Action Program Document (Condition Report)

CEDE

Committed Effective Dose Equivalent

CFR

Code of Federal Regulations

CoC

Certificate of Compliance

DRP

Division of Reactor Projects

DRS

Division of Reactor Safety

EDG

Emergency Diesel Generator

EOP

Emergency Operating Procedure

EPRI

Electric Power Research Institute

FSAR

Final Safety Analysis Report

IEEE

Institute of Electrical & Electronic Engineers

IMC

Inspection Manual Chapter

IP

Inspection Procedure

ips

Inches Per Second

IR

Inspection Report

ISI

Inservice Inspection

IST

Inservice Test

IV

Independent Verification

JPM

Job Performance Measure

kV

Kilovolt

kW

Kilowatt

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LHRA

Locked High Radiation Area

LOCA

Loss of Coolant Accident

LOOP

Loss of Off-site Power

LORT

Licensed Operator Requalification Training

MG

Motor-Generator

MOV

Motor-Operated Valve

mrem

Millirem

MSPI

Mitigating Systems Performance Index

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NIOSH

National Institute of Safety & Health

NMC

Nuclear Management Corporation

NRC

U.S. Nuclear Regulatory Commission

ODCM

Offsite Dose Calculation Manual

OM

Operational Maintenance

OPR

Operability Evaluation

OWA

Operator Workaround

PI

Performance Indicator

PI&R

Problem Identification and Resolution

PM

Planned or Preventative Maintenance

16

Attachment

PMT

Post-Maintenance Testing

ppm

Parts Per Million

PRA

Probabilistic Risk Assessment

QA

Quality Assurance

RCA

Radiologically Controlled Area

RCE

Root Cause Evaluation

RETS

Radiological Effluent Technical Specification

RHR

Residual Heat Removal

RP

Radiation Protection

RPS

Reactor Protection System

RPV

Reactor Pressure Vessel

RWST

Refueling Water Storage Tank

SAT

Systems Approach to Training

SCBA

Self-Contained Breathing Apparatus

SDP

Significance Determination Process

SSC

Structure, System, or Component

SW

Service Water

TDAFW

Turbine-Driven Auxiliary Feedwater

TS

Technical Specification

URI

Unresolved Item

WO

Work Order

VIO

Violation