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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:February 11, 2010  
                                NUC LE AR RE G UL AT O RY C O M M I S S I O N
EA-10-004  
                                                  R E GI ON I V
EA-10-020  
                                      612 EAST LAMAR BLVD , SU I TE 400
Matthew W. Sunseri, President and
                                        AR LI N GTON , TEXAS 76011-4125
   Chief Executive Officer  
                                        February 11, 2010
Wolf Creek Nuclear Operating Corporation  
EA-10-004
P.O. Box 411  
EA-10-020
Burlington, KS 66839  
Matthew W. Sunseri, President and
   Chief Executive Officer
SUBJECT:  
Wolf Creek Nuclear Operating Corporation
WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION  
P.O. Box 411
REPORT 05000482/2009005 AND NOTICE OF VIOLATIONS  
Burlington, KS 66839
Dear Mr. Sunseri:  
SUBJECT:       WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an  
                REPORT 05000482/2009005 AND NOTICE OF VIOLATIONS
inspection at your Wolf Creek Generating Station. The enclosed integrated inspection report  
Dear Mr. Sunseri:
documents the inspection findings, which were discussed on January 14, 2010, with you and  
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
other members of your staff.  
inspection at your Wolf Creek Generating Station. The enclosed integrated inspection report
The inspections examined activities conducted under your license as they relate to safety and  
documents the inspection findings, which were discussed on January 14, 2010, with you and
compliance with the Commissions rules and regulations and with the conditions of your license.
other members of your staff.
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
The inspections examined activities conducted under your license as they relate to safety and
personnel.
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
Based on the results of this inspection, the NRC has identified two issues that were evaluated  
personnel.
under the risk significance determination process as having very low safety significance (green).
Based on the results of this inspection, the NRC has identified two issues that were evaluated
The NRC has also determined that violations are associated with these issues. One violation  
under the risk significance determination process as having very low safety significance (green).
involved failure to implement corrective actions to address refueling water storage tank leakage  
The NRC has also determined that violations are associated with these issues. One violation
(EA-10-004). The second violation involved failure to correct an inadequate reactor vessel head  
involved failure to implement corrective actions to address refueling water storage tank leakage
vent path (EA-10-020). These violations were evaluated in accordance with the NRC  
(EA-10-004). The second violation involved failure to correct an inadequate reactor vessel head
vent path (EA-10-020). These violations were evaluated in accordance with the NRC
Enforcement Policy included on the NRCs Web site at www.nrc.gov/about-
Enforcement Policy included on the NRCs Web site at www.nrc.gov/about-
nrc/regulatory/enforcement/enforce-pol.html.
nrc/regulatory/enforcement/enforce-pol.html.  
The violations are being cited in the enclosed Notice of Violations (Notice) and the
circumstances surrounding them are described in detail in the subject inspection report. The
The violations are being cited in the enclosed Notice of Violations (Notice) and the  
violations are being cited in the Notice because Wolf Creek Generating Station failed to restore
circumstances surrounding them are described in detail in the subject inspection report. The  
compliance within a reasonable time after the violations were identified in NRC Inspection
violations are being cited in the Notice because Wolf Creek Generating Station failed to restore  
Reports 05000482/2007003-006 and 05000482/2008004-007, as specified in Section VI.A.1 of
compliance within a reasonable time after the violations were identified in NRC Inspection  
the NRC Enforcement Policy.
Reports 05000482/2007003-006 and 05000482/2008004-007, as specified in Section VI.A.1 of  
You are required to respond to this letter and should follow the instructions specified in the
the NRC Enforcement Policy.  
enclosed Notice when preparing your response. The NRC will use your response, in part, to
You are required to respond to this letter and should follow the instructions specified in the  
enclosed Notice when preparing your response. The NRC will use your response, in part, to  
UNITED STATES
NUCLEAR REGULATORY COMMISSION
R E GI ON  I V
612 EAST LAMAR BLVD, SUITE 400
ARLINGTON, TEXAS 76011-4125


Wolf Creek Nuclear Operating Corporation - 2 -
Wolf Creek Nuclear Operating Corporation - 2 -
determine whether further enforcement action is necessary to ensure compliance with
regulatory requirements.
Based on the results of this inspection, the NRC has also determined that one additional
- 2 -  
Severity Level IV violation of NRC requirements occurred. This report also documents
determine whether further enforcement action is necessary to ensure compliance with  
12 NRC identified and one self-revealing finding of very low safety significance (Green). All of
regulatory requirements.  
these findings were determined to involve violations of NRC requirements. Additionally, two
Based on the results of this inspection, the NRC has also determined that one additional  
licensee-identified violations, which were determined to be of very low safety significance, are
Severity Level IV violation of NRC requirements occurred. This report also documents  
listed in this report. However, because of the very low safety significance and because they are
12 NRC identified and one self-revealing finding of very low safety significance (Green). All of  
entered into your corrective action program, the NRC is treating these findings as noncited
these findings were determined to involve violations of NRC requirements. Additionally, two  
violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest the
licensee-identified violations, which were determined to be of very low safety significance, are  
violations or the significance of the noncited violations, you should provide a response within
listed in this report. However, because of the very low safety significance and because they are  
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
entered into your corrective action program, the NRC is treating these findings as noncited  
Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with
violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest the  
copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E.
violations or the significance of the noncited violations, you should provide a response within  
Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S.
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident
Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with  
Inspector at the Wolf Creek Generating Station.
copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E.  
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its
Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S.  
enclosure, will be available electronically for public inspection in the NRC Public Document
Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident  
Room or from the Publicly Available Records component of NRCs document system (ADAMS).
Inspector at the Wolf Creek Generating Station.  
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its  
Public Electronic Reading Room).
enclosure, will be available electronically for public inspection in the NRC Public Document  
                                                Sincerely,
Room or from the Publicly Available Records component of NRCs document system (ADAMS).
                                                /RA/
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the  
                                                Geoffrey B. Miller, Chief
Public Electronic Reading Room).  
                                                Project Branch B
                                                Division of Reactor Projects
Sincerely,  
Docket No. 50-482
License No. NPF-42
/RA/  
Enclosure
Inspection Report 05000482/2009005
Geoffrey B. Miller, Chief  
   w/Attachment: Supplemental Information
Project Branch B  
                                            -2-
Division of Reactor Projects  
Docket No. 50-482
License No. NPF-42  
Enclosure  
Inspection Report 05000482/2009005  
   w/Attachment: Supplemental Information  


Wolf Creek Nuclear Operating Corporation - 3 -
Wolf Creek Nuclear Operating Corporation - 3 -  
cc w/Enclosure:
Vice President Operations/Plant Manager       Office of the Governor
Wolf Creek Nuclear Operating Corporation       State of Kansas
- 3 -
P.O. Box 411                                   Topeka, KS 66612
Burlington, KS 66839
cc w/Enclosure:  
                                              Attorney General
Vice President Operations/Plant Manager  
Jay Silberg, Esq.                             120 S.W. 10th Avenue, 2nd Floor
Wolf Creek Nuclear Operating Corporation  
Pillsbury Winthrop Shaw Pittman LLP           Topeka, KS 66612-1597
P.O. Box 411  
2300 N Street, NW
Burlington, KS 66839  
Washington, DC 20037                           County Clerk
                                              Coffey County Courthouse
Jay Silberg, Esq.  
Supervisor Licensing                           110 South 6th Street
Pillsbury Winthrop Shaw Pittman LLP  
Wolf Creek Nuclear Operating Corporation       Burlington, KS 66839
2300 N Street, NW  
P.O. Box 411
Washington, DC 20037  
Burlington, KS 66839                           Chief, Radiation and Asbestos
                                                Control Section
Supervisor Licensing  
Chief Engineer                                Kansas Department of Health and
Wolf Creek Nuclear Operating Corporation  
Utilities Division                              Environment
P.O. Box 411
Kansas Corporation Commission                  Bureau of Air and Radiation
Burlington, KS 66839  
1500 SW Arrowhead Road                        1000 SW Jackson, Suite 310
Topeka, KS 66604-4027                          Topeka, KS 66612-1366
Chief Engineer
                                        -3-
Utilities Division
Kansas Corporation Commission
1500 SW Arrowhead Road
Topeka, KS  66604-4027
Office of the Governor
State of Kansas
Topeka, KS  66612
Attorney General
120 S.W. 10th Avenue, 2nd Floor
Topeka, KS  66612-1597
County Clerk
Coffey County Courthouse
110 South 6th Street
Burlington, KS 66839  
Chief, Radiation and Asbestos  
  Control Section  
Kansas Department of Health and  
  Environment  
Bureau of Air and Radiation  
1000 SW Jackson, Suite 310  
Topeka, KS 66612-1366  


Wolf Creek Nuclear Operating Corporation - 4 -
Wolf Creek Nuclear Operating Corporation - 4 -
Electronic distribution by RIV:
Regional Administrator (Elmo.Collins@nrc.gov)
Deputy Regional Administrator (Chuck.Casto@nrc.gov)
- 4 -  
DRP Director (Dwight.Chamberlain@nrc.gov)
Electronic distribution by RIV:  
DRP Deputy Director (Anton.Vegel@nrc.gov)
Regional Administrator (Elmo.Collins@nrc.gov)  
DRS Director (Roy.Caniano@nrc.gov)
Deputy Regional Administrator (Chuck.Casto@nrc.gov)  
DRS Deputy Director (Troy.Pruett@nrc.gov)
DRP Director (Dwight.Chamberlain@nrc.gov)  
Senior Resident Inspector (Chris.Long@nrc.gov)
DRP Deputy Director (Anton.Vegel@nrc.gov)  
Site Secretary (Shirley.Allen@nrc.gov)
DRS Director (Roy.Caniano@nrc.gov)  
Branch Chief, DRP/B (Geoffrey.Miller@nrc.gov)
DRS Deputy Director (Troy.Pruett@nrc.gov)  
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)
Senior Resident Inspector (Chris.Long@nrc.gov)  
Senior Public Affairs Officer (Victor.Dricks@nrc.gov)
Site Secretary (Shirley.Allen@nrc.gov)  
Senior Public Affairs Officer (Lara.Uselding@nrc.gov)
Branch Chief, DRP/B (Geoffrey.Miller@nrc.gov)  
Public Affairs Officer (Lara.Uselding@nrc.gov)
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)  
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)
Senior Public Affairs Officer (Victor.Dricks@nrc.gov)  
RITS Coordinator (Marisa.Herrera@nrc.gov)
Senior Public Affairs Officer (Lara.Uselding@nrc.gov)  
Only inspection reports to the following:
Public Affairs Officer (Lara.Uselding@nrc.gov)  
DRS/TSB STA (Dale.Powers@nrc.gov)
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)  
L. Trocine, OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)  
ROPreports
File located: R:\_REACTORS\_WC\2009\WC20090005-RP-CML.doc                 ML 100430713
Only inspection reports to the following:  
SUNSI Rev Compl. : Yes No ADAMS                     : Yes No       Reviewer Initials   GBM
DRS/TSB STA (Dale.Powers@nrc.gov)  
Publicly Avail           : Yes No Sensitive           Yes : No     Sens. Type Initials GBM
L. Trocine, OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)  
RI:DRP/                 SRI:DRP/           SPE:DRP/         C:DRS/EB1       C:DRS/EB2
ROPreports  
CAPeabody               CMLong             RDeese           TFarnholtz       NFOKeefe
/RA/GMiller for         /RA/GMiller for /RA/               /RA/             /RA/
01/22/2010             01/29/2010         02/05/2010       02/05/2010       02/05/2010
C:DRS/OB               C:DRS/PSB1         C:DRS/PSB2       RIV:ACES         C:DRP/
SGarchow               MPShannon         GEWerner         RKellar         GBMiller
/RA/                   /RA/               /RA/             /RA/             /RA/
02/09/2010             02/08/2010         02/09/2010       02/09/2010       02/11010
OFFICIAL RECORD COPY T=Telephone                   E=E-mail     F=Fax
                                            -4-
File located: R:\\_REACTORS\\_WC\\2009\\WC20090005-RP-CML.doc       ML 100430713  
SUNSI Rev Compl.  
: Yes No  
ADAMS  
: Yes No  
Reviewer Initials  
GBM
Publicly Avail  
: Yes No  
Sensitive  
Yes : No  
Sens. Type Initials  
GBM
RI:DRP/  
SRI:DRP/  
SPE:DRP/  
C:DRS/EB1  
C:DRS/EB2  
CAPeabody  
CMLong  
RDeese  
TFarnholtz  
NFOKeefe  
/RA/GMiller for  
/RA/GMiller for  
/RA/  
/RA/  
/RA/  
01/22/2010  
01/29/2010  
02/05/2010  
02/05/2010  
02/05/2010  
C:DRS/OB  
C:DRS/PSB1  
C:DRS/PSB2  
RIV:ACES  
C:DRP/  
SGarchow  
MPShannon  
GEWerner  
RKellar  
GBMiller  
/RA/  
/RA/  
/RA/  
/RA/  
/RA/  
02/09/2010  
02/08/2010  
02/09/2010  
02/09/2010  
02/11010  
OFFICIAL RECORD COPY T=Telephone           E=E-mail       F=Fax


                                      NOTICE OF VIOLATIONS
Wolf Creek Nuclear Operating Corporation                                         Docket: 50-482
Wolf Creek Generating Station                                                   License: NPF-42
                                                                                EA-10-004
- 1 -
                                                                                EA-10-020
Enclosure 1
During an NRC inspection conducted October 1 through December 31, 2009, two violations of
NOTICE OF VIOLATIONS  
NRC requirements were identified. In accordance with the NRC Enforcement Policy, the
violations are listed below:
Wolf Creek Nuclear Operating Corporation  
A.       Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,
          in part, that measures shall be established to assure that conditions adverse
          to quality are promptly identified and corrected.
          Contrary to the above, from 1998 to December 31, 2009, the measures
Docket: 50-482  
          established by Wolf Creek did not correct a condition adverse to quality.
Wolf Creek Generating Station  
          Specifically, Wolf Creek did not correct leakage from the refueling water
          storage tank.
License: NPF-42  
          This violation is associated with a Green Significance Determination Process finding
EA-10-004  
          (EA-10-004).
EA-10-020  
B.       Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that
          the design basis is correctly translated into specifications, drawings, and procedures.
During an NRC inspection conducted October 1 through December 31, 2009, two violations of  
          The design basis of the reactor vessel head vent is to allow noncondensable gases to
NRC requirements were identified. In accordance with the NRC Enforcement Policy, the  
          escape to the pressurizer during shutdown conditions.
violations are listed below:  
          Contrary to the above, from December 2, 2003, to December 31, 2009, Wolf Creek
          failed to ensure the design basis of the reactor vessel head vent was correctly translated
A.  
          into specifications, drawings and procedures. Specifically, Wolf Creek designed and
Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,  
          installed a reactor vessel head permanent vent piping modification which failed to vent
in part, that measures shall be established to assure that conditions adverse  
          noncondensable gases to the pressurizer during shutdown operations.
to quality are promptly identified and corrected.  
          This resulted in the formation of voids in the reactor vessel head while the plant was
          shutdown and depressurized in successive refueling outages.
Contrary to the above, from 1998 to December 31, 2009, the measures  
          This violation is associated with a Green Significance Determination Process finding
established by Wolf Creek did not correct a condition adverse to quality.
          (EA-10-020).
Specifically, Wolf Creek did not correct leakage from the refueling water  
Pursuant to the provisions of 10 CFR 2.201, Wolf Creek Nuclear Operating Corporation is
storage tank.
hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory
Commission, ATTN: Document Control Desk, Washington, DC 20555, with a copy to the
This violation is associated with a Green Significance Determination Process finding  
Regional Administrator, Region IV, and a copy to the NRC Senior Resident Inspector at the
(EA-10-004).  
facility that is the subject of this Notice of Violation (Notice), within 30 days of the date of the
B.  
letter transmitting this Notice. This reply should be clearly marked as a "Reply to Notice of
Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that  
Violation EA-10-004," EA 10-020, and should include for each violation (1) the reason for the
the design basis is correctly translated into specifications, drawings, and procedures.
                                                -1-                                Enclosure 1
The design basis of the reactor vessel head vent is to allow noncondensable gases to  
escape to the pressurizer during shutdown conditions.  
Contrary to the above, from December 2, 2003, to December 31, 2009, Wolf Creek  
failed to ensure the design basis of the reactor vessel head vent was correctly translated  
into specifications, drawings and procedures. Specifically, Wolf Creek designed and  
installed a reactor vessel head permanent vent piping modification which failed to vent  
noncondensable gases to the pressurizer during shutdown operations.  
This resulted in the formation of voids in the reactor vessel head while the plant was  
shutdown and depressurized in successive refueling outages.  
This violation is associated with a Green Significance Determination Process finding  
(EA-10-020).
Pursuant to the provisions of 10 CFR 2.201, Wolf Creek Nuclear Operating Corporation is  
hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory  
Commission, ATTN: Document Control Desk, Washington, DC 20555, with a copy to the  
Regional Administrator, Region IV, and a copy to the NRC Senior Resident Inspector at the  
facility that is the subject of this Notice of Violation (Notice), within 30 days of the date of the  
letter transmitting this Notice. This reply should be clearly marked as a "Reply to Notice of  
Violation EA-10-004," EA 10-020, and should include for each violation (1) the reason for the  


violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective
steps that have been taken and the results achieved, (3) the corrective steps
That will be taken to avoid further violations, and (4) the date when full compliance will be
achieved. Your response may reference or include previous docketed correspondence, if the
- 2 -
correspondence adequately addresses the required response. If an adequate reply is not
Enclosure 1
received within the time specified in this Notice, an Order or a Demand for Information may be
violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective  
issued as to why the license should not be modified, suspended, or revoked, or why such other
steps that have been taken and the results achieved, (3) the corrective steps
action as may be proper should not be taken. Where good cause is shown, consideration will
That will be taken to avoid further violations, and (4) the date when full compliance will be  
be given to extending the response time.
achieved. Your response may reference or include previous docketed correspondence, if the  
If you contest this enforcement action, you should also provide a copy of your response, with
correspondence adequately addresses the required response. If an adequate reply is not  
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear
received within the time specified in this Notice, an Order or a Demand for Information may be  
Regulatory Commission, Washington, DC 20555-0001.
issued as to why the license should not be modified, suspended, or revoked, or why such other  
Because your response will be made available electronically for public inspection in the NRC
action as may be proper should not be taken. Where good cause is shown, consideration will  
Public Document Room or from the NRCs document system (ADAMS), accessible from the
be given to extending the response time.  
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not
include any personal privacy, proprietary, or safeguards information so that it can be made
If you contest this enforcement action, you should also provide a copy of your response, with  
available to the public without redaction. If personal privacy or proprietary information is
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear  
necessary to provide an acceptable response, then please provide a bracketed copy of your
Regulatory Commission, Washington, DC 20555-0001.  
response that identifies the information that should be protected and a redacted copy of your
response that deletes such information. If you request withholding of such material, you must
Because your response will be made available electronically for public inspection in the NRC  
specifically identify the portions of your response that you seek to have withheld and provide in
Public Document Room or from the NRCs document system (ADAMS), accessible from the  
detail the bases for your claim of withholding (e.g., explain why the disclosure of information will
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not  
create an unwarranted invasion of personal privacy or provide the information required by
include any personal privacy, proprietary, or safeguards information so that it can be made  
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial
available to the public without redaction. If personal privacy or proprietary information is  
information. If safeguards information is necessary to provide an acceptable response, please
necessary to provide an acceptable response, then please provide a bracketed copy of your  
provide the level of protection described in 10 CFR 73.21.
response that identifies the information that should be protected and a redacted copy of your  
Dated this 11h day of February 2010
response that deletes such information. If you request withholding of such material, you must  
                                              -2-                                  Enclosure 1
specifically identify the portions of your response that you seek to have withheld and provide in  
detail the bases for your claim of withholding (e.g., explain why the disclosure of information will  
create an unwarranted invasion of personal privacy or provide the information required by  
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial  
information. If safeguards information is necessary to provide an acceptable response, please  
provide the level of protection described in 10 CFR 73.21.  
Dated this 11h day of February 2010  


                  U.S. NUCLEAR REGULATORY COMMISSION
                                      REGION IV
Docket:     05000482
- 1 -
License:     NPF-42
Report:     05000482/2009005
Licensee:   Wolf Creek Operating Corporation
Facility:   Wolf Creek Generating Station
Location:   1550 Oxen Lane SE
Enclosure 2
            Burlington, Kansas
U.S. NUCLEAR REGULATORY COMMISSION  
Dates:       October 1 through December 31, 2009
REGION IV  
Inspectors: C. M. Long, Senior Resident Inspector
            R. A. Kopriva, Senior Reactor Inspector
Docket:  
            J. F. Drake, Senior Reactor Inspector
05000482  
            D. Loveless, Senior Reactor Analyst
License:  
            C. A. Peabody, Resident Inspector
NPF-42  
            S. M. Alferink, Reactor Inspector
Report:  
            P. A. Jayroe, Project Engineer
05000482/2009005  
            C. Cauffman, Operations Engineer
Licensee:  
            A. L. Fairbanks, Reactor Inspector
Wolf Creek Operating Corporation  
            C. C. Alldredge, Project Engineer
Facility:  
            G. M. Vasquez, Senior Health Physicist
Wolf Creek Generating Station  
            D. C. Graves, Health Physicist
Location:  
Approved By: G. B. Miller, Chief, Project Branch B
1550 Oxen Lane SE  
            Division of Reactor Projects
Burlington, Kansas  
                                      -1-            Enclosure 2
Dates:  
October 1 through December 31, 2009  
Inspectors:  
C. M. Long, Senior Resident Inspector  
R. A. Kopriva, Senior Reactor Inspector  
J. F. Drake, Senior Reactor Inspector  
D. Loveless, Senior Reactor Analyst  
C. A. Peabody, Resident Inspector  
S. M. Alferink, Reactor Inspector  
P. A. Jayroe, Project Engineer  
C. Cauffman, Operations Engineer  
A. L. Fairbanks, Reactor Inspector
C. C. Alldredge, Project Engineer  
G. M. Vasquez, Senior Health Physicist  
D. C. Graves, Health Physicist  
Approved By:  
G. B. Miller, Chief, Project Branch B  
Division of Reactor Projects  


                                      SUMMARY OF FINDINGS
IR 05000482/2008005, 10/01/2009 - 12/31/2009; Wolf Creek Generating Station, Integrated
Resident and Regional Report; Fire Protection, Inservice Inspection Activities; Maintenance Risk
- 2 -
Assessments and Emergent Work Controls; Operability Evaluations; Plant Modifications;
Refueling Outage and Other Outage Activities; Radiation Safety; Identification and Resolution of
Problems, and Other Activities.
The report covered a 3-month period of inspection by resident inspectors and an announced
baseline inspections by a regional based inspectors. Fourteen Green and one Severity Level IV
Enclosure 2
noncited violation were identified and two Green cited violations were also identified. The
SUMMARY OF FINDINGS  
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
IR 05000482/2008005, 10/01/2009 - 12/31/2009; Wolf Creek Generating Station, Integrated  
Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the
Resident and Regional Report; Fire Protection, Inservice Inspection Activities; Maintenance Risk  
significance determination process does not apply may be Green or be assigned a severity level
Assessments and Emergent Work Controls; Operability Evaluations; Plant Modifications;  
after NRC management review. The NRC's program for overseeing the safe operation of
Refueling Outage and Other Outage Activities; Radiation Safety; Identification and Resolution of  
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,
Problems, and Other Activities.  
Revision 4, dated December 2006.
The report covered a 3-month period of inspection by resident inspectors and an announced  
A.     NRC-Identified Findings and Self-Revealing Findings
baseline inspections by a regional based inspectors. Fourteen Green and one Severity Level IV
        Cornerstone: Initiating Events
noncited violation were identified and two Green cited violations were also identified. The  
*     Green. The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B,
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using  
        Criterion V, Instructions, Procedures, and Drawings, involving the licensees failure to
Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the  
        identify sources of boron leakage and document them in a corrective action document.
significance determination process does not apply may be Green or be assigned a severity level  
        Specifically, prior to October 23, 2009, the licensee failed to accomplish the
after NRC management review. The NRC's program for overseeing the safe operation of  
        requirements of Procedure AP 16F-001, Boric Acid Corrosion Control Program,
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,  
        Revision 5, step 6.4.1, which states, in part, Sources of boron seepage/leakage shall
Revision 4, dated December 2006.  
        be identified/verified and documented in the applicable corrective action document.
A.  
        During a boric acid walkdown, the inspectors identified 11 sources of boron leakage
NRC-Identified Findings and Self-Revealing Findings  
        which had not been previously identified and documented by the licensee. The licensee
Cornerstone: Initiating Events  
        entered this finding into their corrective action system as Condition Report 00021274.
*  
        The finding was determined to be more than minor because it was associated with the
Green. The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B,  
        Initiating Events Cornerstone attribute of human performance and affected the
Criterion V, Instructions, Procedures, and Drawings, involving the licensees failure to  
        cornerstone objective to limit the likelihood of those events that upset plant stability and
identify sources of boron leakage and document them in a corrective action document.
        challenge critical safety functions during shutdown as well as power operations. The
Specifically, prior to October 23, 2009, the licensee failed to accomplish the  
        inspectors used Inspection Manual Chapter 0609, Significance Determination Process,
requirements of Procedure AP 16F-001, Boric Acid Corrosion Control Program,  
        Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, and
Revision 5, step 6.4.1, which states, in part, Sources of boron seepage/leakage shall  
        determined the finding was of very low safety significance (Green) because the issue
be identified/verified and documented in the applicable corrective action document.
        would not result in exceeding the technical specification limit for identified reactor
During a boric acid walkdown, the inspectors identified 11 sources of boron leakage  
        coolant system leakage or affect other mitigating systems resulting in a total loss of their
which had not been previously identified and documented by the licensee. The licensee  
        safety function. The inspectors also determined that the finding had a crosscutting
entered this finding into their corrective action system as Condition Report 00021274.  
        aspect in the area of problem identification and resolution, operating experience, where
The finding was determined to be more than minor because it was associated with the  
        the licensee did not institutionalize operating experience through changes to station
Initiating Events Cornerstone attribute of human performance and affected the  
        processes, procedures, equipment, and training programs [P.2.(b)] (Section 1R08.2.b).
cornerstone objective to limit the likelihood of those events that upset plant stability and  
                                              -2-                                      Enclosure 2
challenge critical safety functions during shutdown as well as power operations. The  
inspectors used Inspection Manual Chapter 0609, Significance Determination Process,  
Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, and  
determined the finding was of very low safety significance (Green) because the issue  
would not result in exceeding the technical specification limit for identified reactor  
coolant system leakage or affect other mitigating systems resulting in a total loss of their  
safety function. The inspectors also determined that the finding had a crosscutting  
aspect in the area of problem identification and resolution, operating experience, where  
the licensee did not institutionalize operating experience through changes to station  
processes, procedures, equipment, and training programs [P.2.(b)] (Section 1R08.2.b).  


* Green. On December 16, 2009, inspectors identified a noncited violation of 10 CFR
  Part 50, Appendix B, Criterion III, Design Control, involving failure to obtain vendor
  design data for a modification. In August 2009, a component cooling water modification
- 3 -
  was made to the reactor coolant pump thermal barrier heat exchangers flow rates as a
  corrective action to VIO 05000482/2009002 07 (EA-09-110). A flow rate above the
  previous design value was justified by an internal memo of a vendor opinion from a
  telephone conversation in 1992. The inspectors found this to be contrary to
  Procedure AP 05-005, for obtaining data from vendors. The notice of violation will
Enclosure 2
  remain open until full compliance has been restored. Wolf Creek consulted with
*  
  Westinghouse, confirmed the acceptability of the increased flow rate, and requested a
Green. On December 16, 2009, inspectors identified a noncited violation of 10 CFR  
  formal calculation. This issue is captured in Condition Report 22824.
Part 50, Appendix B, Criterion III, Design Control, involving failure to obtain vendor  
  The inspectors determined that this finding was more than minor because this issue
design data for a modification. In August 2009, a component cooling water modification  
  aligned with Inspection Manual Chapter 0612, Appendix E, example 2.f, in that the
was made to the reactor coolant pump thermal barrier heat exchangers flow rates as a  
  modification relied on verbal statements to raise the allowable flow through the heat
corrective action to VIO 05000482/2009002 07 (EA-09-110). A flow rate above the  
  exchanger. This is a significant deficiency in the modification package. The inspectors
previous design value was justified by an internal memo of a vendor opinion from a  
  determined this finding was associated with the design control attribute of the Initiating
telephone conversation in 1992. The inspectors found this to be contrary to  
  Events Cornerstone and affected the cornerstone objective to limit the likelihood of
Procedure AP 05-005, for obtaining data from vendors. The notice of violation will  
  events that upset plant stability and challenge critical safety functions. The inspectors
remain open until full compliance has been restored. Wolf Creek consulted with  
  evaluated the significance of this finding using Phase 1 of Inspection Manual
Westinghouse, confirmed the acceptability of the increased flow rate, and requested a  
  Chapter 0609.04 and determined that the finding was of very low safety significance
formal calculation. This issue is captured in Condition Report 22824.  
  because assuming worst case degradation, the finding would not result in exceeding the
The inspectors determined that this finding was more than minor because this issue  
  technical specification limit for identified reactor coolant system leakage and would not
aligned with Inspection Manual Chapter 0612, Appendix E, example 2.f, in that the  
  have likely affected other mitigation systems resulting in a total loss of their safety
modification relied on verbal statements to raise the allowable flow through the heat  
  function because seal injection was available. This finding has a crosscutting aspect in
exchanger. This is a significant deficiency in the modification package. The inspectors  
  the area of human performance associated with work practices in that management was
determined this finding was associated with the design control attribute of the Initiating  
  unsuccessful in communicating expectations on procedure use and adherence in
Events Cornerstone and affected the cornerstone objective to limit the likelihood of  
  engineering [H.4.b] (Section 1R18).
events that upset plant stability and challenge critical safety functions. The inspectors  
* Green. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,
evaluated the significance of this finding using Phase 1 of Inspection Manual  
  Criterion III, Design Control, due to an inadequate vent path for the reactor vessel
Chapter 0609.04 and determined that the finding was of very low safety significance  
  head. The inadequate vent path resulted in the formation of voids in the reactor vessel
because assuming worst case degradation, the finding would not result in exceeding the  
  head during Refueling Outage 17. Failure to ensure an adequate vent path in the
technical specification limit for identified reactor coolant system leakage and would not  
  reactor vessel head was the subject of a noncited violation in NRC Inspection
have likely affected other mitigation systems resulting in a total loss of their safety  
  Report 05000482/2008004. During and after Refueling Outage 16, Wolf Creek initiated
function because seal injection was available. This finding has a crosscutting aspect in  
  a root cause evaluation and corrective actions to prevent occurrence. When one of the
the area of human performance associated with work practices in that management was  
  possible root causes was disproven in Refueling Outage 17, no additional action was
unsuccessful in communicating expectations on procedure use and adherence in  
  taken to determine the cause of the vessel head vent blockage. However, the licensee
engineering [H.4.b] (Section 1R18).  
  could not exclude blockage in the piping. This issue was entered into the corrective
*  
  action program and the licensee plans to conduct a more thorough inspection of the
Green. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,  
  piping during the next refueling outage. This issue is being tracked by the licensee as
Criterion III, Design Control, due to an inadequate vent path for the reactor vessel  
  Condition Report 22501.
head. The inadequate vent path resulted in the formation of voids in the reactor vessel  
  The inspectors determined that the failure to provide adequate vessel head vent path to
head during Refueling Outage 17. Failure to ensure an adequate vent path in the  
  prevent gas accumulation in the reactor vessel during depressurized plant operations
reactor vessel head was the subject of a noncited violation in NRC Inspection  
  was a performance deficiency. The inspectors determined that this finding, which was
Report 05000482/2008004. During and after Refueling Outage 16, Wolf Creek initiated  
  associated with the Initiating Events Cornerstone, was more than minor because if left
a root cause evaluation and corrective actions to prevent occurrence. When one of the  
  uncorrected, it would have become a more significant-safety concern. Specifically,
possible root causes was disproven in Refueling Outage 17, no additional action was  
                                        -3-                                      Enclosure 2
taken to determine the cause of the vessel head vent blockage. However, the licensee  
could not exclude blockage in the piping. This issue was entered into the corrective  
action program and the licensee plans to conduct a more thorough inspection of the  
piping during the next refueling outage. This issue is being tracked by the licensee as  
Condition Report 22501.  
The inspectors determined that the failure to provide adequate vessel head vent path to  
prevent gas accumulation in the reactor vessel during depressurized plant operations  
was a performance deficiency. The inspectors determined that this finding, which was  
associated with the Initiating Events Cornerstone, was more than minor because if left  
uncorrected, it would have become a more significant-safety concern. Specifically,  


  without an adequate vent path the reactor vessel does not have an effective means of
  relieving noncondensable gases to prevent a loss of reactor coolant system inventory.
  The inspectors evaluated this finding using Inspection Manual Chapter 0609,
- 4 -
  Appendix G, Attachment 1, and determined it be of very low safety significance based
  upon the demonstrated availability of mitigating systems and the flooded reactor cavity
  inventory. The inspectors determined the cause of the finding had a problem
  identification and resolution aspect in the corrective action program. Specifically, Wolf
  Creeks corrective actions were not successful to address the vent path blockage in a
Enclosure 2
  timely manner [P.1(d)] (Section 1R20).
without an adequate vent path the reactor vessel does not have an effective means of  
* Green. The inspectors identified a noncited violation of License Condition 2.C.(5), Fire
relieving noncondensable gases to prevent a loss of reactor coolant system inventory.
  Protection, for the failure to implement and maintain the approved fire protection
The inspectors evaluated this finding using Inspection Manual Chapter 0609,  
  program. Specifically, the licensee prescribed mitigating actions in response to certain
Appendix G, Attachment 1, and determined it be of very low safety significance based  
  fire scenarios that would result in a loss of circuit breaker coordination and could initiate
upon the demonstrated availability of mitigating systems and the flooded reactor cavity  
  secondary fires in plant locations outside of the initial fire area. The licensee entered
inventory. The inspectors determined the cause of the finding had a problem  
  this issue into their corrective action program as Condition Report 2008-005210.
identification and resolution aspect in the corrective action program. Specifically, Wolf  
  This finding was more than minor because it was associated with the Protection Against
Creeks corrective actions were not successful to address the vent path blockage in a  
  External Factors attribute of the Initiating Events Cornerstone and adversely affected the
timely manner [P.1(d)] (Section 1R20).  
  cornerstone objective to limit the likelihood of those events that upset plant stability and
*  
  challenge critical safety functions during shutdown as well as power operations. The
Green. The inspectors identified a noncited violation of License Condition 2.C.(5), Fire  
  risk significance of this finding was determined using Manual Chapter 0609, Appendix F,
Protection, for the failure to implement and maintain the approved fire protection  
  Fire Protection Significance Determination Process. The finding was determined to be
program. Specifically, the licensee prescribed mitigating actions in response to certain  
  of very low safety significance using a Phase 2 evaluation. This finding was not
fire scenarios that would result in a loss of circuit breaker coordination and could initiate  
  assigned a crosscutting aspect because the cause was not representative of current
secondary fires in plant locations outside of the initial fire area. The licensee entered  
  performance (Section 4OA5.2).
this issue into their corrective action program as Condition Report 2008-005210.  
  Cornerstone: Mitigating Systems
* Green. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,
This finding was more than minor because it was associated with the Protection Against  
  Criterion XVI, Corrective Action, for failure to take action to stop leakage from the base
External Factors attribute of the Initiating Events Cornerstone and adversely affected the  
  of the refueling water storage tank or evaluate the leakage and wastage for
cornerstone objective to limit the likelihood of those events that upset plant stability and  
  acceptability. Specifically, the licensee did not take actions to prevent recurring
challenge critical safety functions during shutdown as well as power operations. The  
  discolored boric acid deposits for approximately 11 years. Failure to correct leakage
risk significance of this finding was determined using Manual Chapter 0609, Appendix F,  
  from the refueling water storage tank base was the subject of a noncited violation in
Fire Protection Significance Determination Process. The finding was determined to be  
  NRC Inspection Report 05000482/2007006. This issue was entered into the licensee's
of very low safety significance using a Phase 2 evaluation. This finding was not  
  corrective action program as Condition Report 22866.
assigned a crosscutting aspect because the cause was not representative of current  
  The failure to implement corrective actions for the refueling water storage tank leakage
performance (Section 4OA5.2).  
  was a performance deficiency. The inspectors determined this issue impacted the
Cornerstone: Mitigating Systems  
  Mitigating Systems Cornerstone and was greater than minor because if left uncorrected,
  the failure to correct the presence of boric acid leakage could become a more significant
*  
  safety concern in that continued wastage could impact tank operability. Using the
Green. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,  
  Phase 1 worksheets in Inspection Manual Chapter 0609.04, "Significance Determination
Criterion XVI, Corrective Action, for failure to take action to stop leakage from the base  
  Process," the finding was determined to have very low safety significance because it did
of the refueling water storage tank or evaluate the leakage and wastage for  
  not result in a system or component being inoperable and it did not screen as potentially
acceptability. Specifically, the licensee did not take actions to prevent recurring  
  risk significant due to a seismic, flooding, or severe weather initiating event. The
discolored boric acid deposits for approximately 11 years. Failure to correct leakage  
  inspectors identified a crosscutting aspect in the area of human performance associated
from the refueling water storage tank base was the subject of a noncited violation in  
                                        -4-                                      Enclosure 2
NRC Inspection Report 05000482/2007006. This issue was entered into the licensee's  
corrective action program as Condition Report 22866.
The failure to implement corrective actions for the refueling water storage tank leakage  
was a performance deficiency. The inspectors determined this issue impacted the  
Mitigating Systems Cornerstone and was greater than minor because if left uncorrected,  
the failure to correct the presence of boric acid leakage could become a more significant  
safety concern in that continued wastage could impact tank operability. Using the  
Phase 1 worksheets in Inspection Manual Chapter 0609.04, "Significance Determination  
Process," the finding was determined to have very low safety significance because it did  
not result in a system or component being inoperable and it did not screen as potentially  
risk significant due to a seismic, flooding, or severe weather initiating event. The  
inspectors identified a crosscutting aspect in the area of human performance associated  


  with resources. Specifically, Wolf Creek did not maintain long-term plant safety
  minimizing corrective maintenance deferrals and this long-standing equipment issue
  [H.2.c] (Section 1R05).
- 5 -
* Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a,
  for an inadequate Procedure AP-10-101, Control of Transient Ignition Sources. On
  October 21, 2009, the inspectors observed maintenance personnel performing weld
  preparation work on essential service water piping to containment cooler B using a
  flapper wheel. The inspectors observed that the ignition control barriers for the hot work
Enclosure 2
  were insufficient in that the sparks from the preparation work extended four to five feet
with resources. Specifically, Wolf Creek did not maintain long-term plant safety  
  from the job site and there was no fire watch posted. On December 4, 2003, a
minimizing corrective maintenance deferrals and this long-standing equipment issue  
  procedure revision inappropriately incorporated a change to the procedure where a fire
[H.2.c] (Section 1R05).  
  watch did not have to be posted when using wire brushes, flapper wheels, polishing
  devices, or Rol-Lok type buffing pads mounted on power grinder motor drives or air
*  
  tools. The maintenance supervisor stopped the work until a fire watch was posted. The
Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a,  
  licensee entered this into their corrective action system as Condition Report 20993.
for an inadequate Procedure AP-10-101, Control of Transient Ignition Sources. On  
  This finding is more than minor because it affected the Mitigating Systems Cornerstone
October 21, 2009, the inspectors observed maintenance personnel performing weld  
  attribute of Protection Against External Factors - Fires, and adversely affected the
preparation work on essential service water piping to containment cooler B using a  
  cornerstone objective to ensure the availability, reliability, and capability of systems that
flapper wheel. The inspectors observed that the ignition control barriers for the hot work  
  respond to initiating events to prevent undesirable consequences. The lack of a posted
were insufficient in that the sparks from the preparation work extended four to five feet  
  fire watch could adversely affect the ability to achieve and maintain safe shutdown in the
from the job site and there was no fire watch posted. On December 4, 2003, a  
  event of a severe fire in the affected area. Inspection Manual Chapter 0609,
procedure revision inappropriately incorporated a change to the procedure where a fire  
  Appendix F, Fire Protection Significance Determination Process, could not be used to
watch did not have to be posted when using wire brushes, flapper wheels, polishing  
  effectively evaluate the finding and defense-in-depth strategies because the 2003
devices, or Rol-Lok type buffing pads mounted on power grinder motor drives or air  
  changes to the fire watch program affected multiple fire areas and conditions. Therefore,
tools. The maintenance supervisor stopped the work until a fire watch was posted. The  
  in accordance with Inspection Manual Chapter 0609, Appendix M, the safety significance
licensee entered this into their corrective action system as Condition Report 20993.  
  was determined by regional management review who concluded that the finding was of
  very low safety significance (Green). This finding was reviewed for crosscutting aspects
This finding is more than minor because it affected the Mitigating Systems Cornerstone  
  and none were identified. The original change occurred in 2003 and was not indicative
attribute of Protection Against External Factors - Fires, and adversely affected the  
  of current performance (Section 1R05.2).
cornerstone objective to ensure the availability, reliability, and capability of systems that  
* Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(4) involving the
respond to initiating events to prevent undesirable consequences. The lack of a posted  
  failure to adequately perform shutdown risk assessments during Refueling Outage 17.
fire watch could adversely affect the ability to achieve and maintain safe shutdown in the  
  Between October 10 and November 17, 2009, Wolf Creek did not appropriately consider
event of a severe fire in the affected area. Inspection Manual Chapter 0609,  
  electrical power, decay heat removal, and containment when assessing shutdown risk.
Appendix F, Fire Protection Significance Determination Process, could not be used to  
  This changed the outcome or color of the qualitative calculation on several occasions.
effectively evaluate the finding and defense-in-depth strategies because the 2003  
  The licensee entered this issue in their corrective action program as Condition
changes to the fire watch program affected multiple fire areas and conditions. Therefore,  
  Reports 22295 and 22296.
in accordance with Inspection Manual Chapter 0609, Appendix M, the safety significance  
  The failure to meet shutdown risk assessment requirements in the daily shutdown risk
was determined by regional management review who concluded that the finding was of  
  assessment process is a performance deficiency. The inspectors determined this finding
very low safety significance (Green). This finding was reviewed for crosscutting aspects  
  was associated with the Mitigating Systems Cornerstone and was more than minor
and none were identified. The original change occurred in 2003 and was not indicative  
  because it involved incorrect risk assessment assumptions by omitting requirements
of current performance (Section 1R05.2).  
  specified in committed guidance without providing justification for that omission. Such
*  
  errors of omission have the potential to change the outcome of the licensees
Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(4) involving the  
  maintenance risk assessment as described above. Per Inspection Manual
failure to adequately perform shutdown risk assessments during Refueling Outage 17.
                                        -5-                                      Enclosure 2
Between October 10 and November 17, 2009, Wolf Creek did not appropriately consider  
electrical power, decay heat removal, and containment when assessing shutdown risk.
This changed the outcome or color of the qualitative calculation on several occasions.
The licensee entered this issue in their corrective action program as Condition  
Reports 22295 and 22296.  
The failure to meet shutdown risk assessment requirements in the daily shutdown risk  
assessment process is a performance deficiency. The inspectors determined this finding  
was associated with the Mitigating Systems Cornerstone and was more than minor  
because it involved incorrect risk assessment assumptions by omitting requirements  
specified in committed guidance without providing justification for that omission. Such  
errors of omission have the potential to change the outcome of the licensees  
maintenance risk assessment as described above. Per Inspection Manual  


  Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management
  Significance Determination Process, licensees who only perform qualitative analyses of
  plant configuration risk due to maintenance activities, the significance of the deficiencies
- 6 -
  must be determined by an internal NRC management review using risk insights where
  possible in accordance with Inspection Manual Chapter 612, Power Reactor Inspection
  Reports. The NRC management review concluded that this finding was of Green safety
  significance because missing risk management actions did not result in loss of key
  shutdown risk functions. Additionally, the cause of the finding has a human performance
Enclosure 2
  crosscutting aspect in the area associated with the resources. Specifically, Wolf Creek
Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management  
  did not ensure that Procedure APF 22B-001-02 was complete, accurate, and up-to-date
Significance Determination Process, licensees who only perform qualitative analyses of  
  [H.2(c)] (Section 1R13).
plant configuration risk due to maintenance activities, the significance of the deficiencies  
* Green. On November 18, 2009, the inspectors identified a noncited violation of
must be determined by an internal NRC management review using risk insights where  
  Technical Specification 3.0.4.b for ascension from Mode 4 to Mode 3 without establishing
possible in accordance with Inspection Manual Chapter 612, Power Reactor Inspection  
  required risk management actions. Wolf Creek used technical specification Limiting
Reports. The NRC management review concluded that this finding was of Green safety  
  Condition for Operation 3.0.4.b to permit mode ascension after performance of a risk
significance because missing risk management actions did not result in loss of key  
  assessment and identification of risk management actions to maintain safety in the next
shutdown risk functions. Additionally, the cause of the finding has a human performance  
  mode. The turbine-driven auxiliary feedwater pump was inoperable per Technical
crosscutting aspect in the area associated with the resources. Specifically, Wolf Creek  
  Specification 3.7.5. As a risk management action, protected train signs would be placed
did not ensure that Procedure APF 22B-001-02 was complete, accurate, and up-to-date  
  on the doors to the motor-driven auxiliary feedwater Pump A and B room doors. A
[H.2(c)] (Section 1R13).
  walkdown conducted by the inspector on the morning of November 18, 2009, found that
*  
  the protected train signs on the motor-driven auxiliary feedwater pump rooms were not in
Green. On November 18, 2009, the inspectors identified a noncited violation of  
  place. Also, a maintenance crew was performing radiography in the motor-driven
Technical Specification 3.0.4.b for ascension from Mode 4 to Mode 3 without establishing  
  auxiliary feedwater pump Room B. The motor-driven auxiliary feedwater Pumps A and B
required risk management actions. Wolf Creek used technical specification Limiting  
  were also made inoperable (at separate times) later on the morning of November 18,
Condition for Operation 3.0.4.b to permit mode ascension after performance of a risk  
  2009. The licensee entered this issue in their corrective action program as Condition
assessment and identification of risk management actions to maintain safety in the next  
  Report 21926.
mode. The turbine-driven auxiliary feedwater pump was inoperable per Technical  
  Mode ascension under Technical Specification LCO 3.0.4.b without establishing required
Specification 3.7.5. As a risk management action, protected train signs would be placed  
  risk management actions is a performance deficiency. The finding was more than minor
on the doors to the motor-driven auxiliary feedwater Pump A and B room doors. A  
  because it was associated with the configuration control and alignment attribute of the
walkdown conducted by the inspector on the morning of November 18, 2009, found that  
  Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the
the protected train signs on the motor-driven auxiliary feedwater pump rooms were not in  
  availability, reliability, and capability of systems that respond to initiating events to
place. Also, a maintenance crew was performing radiography in the motor-driven  
  prevent undesirable consequences. The configuration control issues not only included
auxiliary feedwater pump Room B. The motor-driven auxiliary feedwater Pumps A and B  
  the work being completed on the turbine-driven auxiliary feedwater pump, but also
were also made inoperable (at separate times) later on the morning of November 18,  
  included containment isolation valve testing and radiography that was performed on the
2009. The licensee entered this issue in their corrective action program as Condition  
  motor-driven auxiliary feedwater pumps which was not included in the risk assessment.
Report 21926.  
  The inspector used Inspection Manual Chapter 0609.04, to determine that the finding
Mode ascension under Technical Specification LCO 3.0.4.b without establishing required  
  was of very-low safety significance (Green) because it did not result in a loss of system
risk management actions is a performance deficiency. The finding was more than minor  
  safety function; did not exceed allowable technical specification outage time; and was
because it was associated with the configuration control and alignment attribute of the  
  not a seismic, flooding, or severe weather concern. Additionally, the cause of the finding
Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the  
  has a human performance crosscutting aspect in the area associated with decision
availability, reliability, and capability of systems that respond to initiating events to  
  making. Specifically, Wolf Creek used a risk assessment form and an informal mode
prevent undesirable consequences. The configuration control issues not only included  
  change form to communicate between departments the requirement for risk
the work being completed on the turbine-driven auxiliary feedwater pump, but also  
  management actions. The two forms were in conflict and the personnel who
included containment isolation valve testing and radiography that was performed on the  
  implemented the risk management actions were not informed [H.1(c)] (Section 1R13).
motor-driven auxiliary feedwater pumps which was not included in the risk assessment.
                                          -6-                                      Enclosure 2
The inspector used Inspection Manual Chapter 0609.04, to determine that the finding  
was of very-low safety significance (Green) because it did not result in a loss of system  
safety function; did not exceed allowable technical specification outage time; and was  
not a seismic, flooding, or severe weather concern. Additionally, the cause of the finding  
has a human performance crosscutting aspect in the area associated with decision  
making. Specifically, Wolf Creek used a risk assessment form and an informal mode  
change form to communicate between departments the requirement for risk  
management actions. The two forms were in conflict and the personnel who  
implemented the risk management actions were not informed [H.1(c)] (Section 1R13).  


* Green. On October 15, 2009, the inspectors identified a noncited violation of 10 CFR
  Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to
  follow Procedure AP 28A-100, Condition Reports. Wolf Creek failed to initiate a
- 7 -
  condition report for evaluation of corrosion on containment cooler A piping. After
  inspector challenging, Wolf Creek initiated condition reports, performed nondestructive
  testing, replaced corroded studs, and evaluated the cause of the corrosion.
  The inspectors determined that the failure to follow AP 28A-100, Appendix C, was a
  performance deficiency. This issue was more than minor because it was associated
Enclosure 2
  with the equipment performance attribute of the Mitigating Systems Cornerstone and
*  
  affected the cornerstone objective to ensure the availability, reliability, and capability of
Green. On October 15, 2009, the inspectors identified a noncited violation of 10 CFR  
  systems that respond to initiating events to prevent undesirable consequences. Using
Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to  
  Inspection Manual Chapter 0609.04, the issue screened to Green because there was
follow Procedure AP 28A-100, Condition Reports. Wolf Creek failed to initiate a  
  not a loss of operability and the finding did not screen as potentially risk significant due
condition report for evaluation of corrosion on containment cooler A piping. After  
  to a seismic, flooding, or severe weather initiating event. A crosscutting aspect was
inspector challenging, Wolf Creek initiated condition reports, performed nondestructive  
  identified in the problem identification and resolution area of the corrective action
testing, replaced corroded studs, and evaluated the cause of the corrosion.
  program. Specifically, Wolf Creek failed to implement a corrective action program with a
The inspectors determined that the failure to follow AP 28A-100, Appendix C, was a  
  low threshold for identifying issues [P.1.a] (Section 1R13).
performance deficiency. This issue was more than minor because it was associated  
* Green. On November 23, 2009, a self-revealing violation of Technical
with the equipment performance attribute of the Mitigating Systems Cornerstone and  
    Specification 5.4.1.a was identified when a technician failed to follow procedure and
affected the cornerstone objective to ensure the availability, reliability, and capability of  
    emptied 45 gallons of oil from centrifugal charging Pump A rendering the pump
systems that respond to initiating events to prevent undesirable consequences. Using  
    inoperable. The technician was supposed to remove the temperature indicator for
Inspection Manual Chapter 0609.04, the issue screened to Green because there was  
    calibration but instead removed the thermowell which breached the lube oil subsystem
not a loss of operability and the finding did not screen as potentially risk significant due  
    of centrifugal charging Pump A. An unplanned entry into Technical Specification 3.5.2,
to a seismic, flooding, or severe weather initiating event. A crosscutting aspect was  
    Condition A, was made for approximately 10 hours. The licensee entered this issue in
identified in the problem identification and resolution area of the corrective action  
    their corrective action program as Condition Report 21993.
program. Specifically, Wolf Creek failed to implement a corrective action program with a  
  The failure to follow station procedures and correctly remove the detector was a
low threshold for identifying issues [P.1.a] (Section 1R13).  
  performance deficiency. The finding was more than minor because it was associated
*  
  with the equipment performance attribute of the Mitigating Systems Cornerstone and
Green. On November 23, 2009, a self-revealing violation of Technical  
  affected the cornerstone objective to ensure the availability, reliability, and capability of
Specification 5.4.1.a was identified when a technician failed to follow procedure and  
  systems that respond to initiating events to prevent undesirable consequences. The
emptied 45 gallons of oil from centrifugal charging Pump A rendering the pump  
  inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual
inoperable. The technician was supposed to remove the temperature indicator for  
  Chapter 0609.04, and determined that the finding was of very low safety significance
calibration but instead removed the thermowell which breached the lube oil subsystem  
  (Green) because the pump was inoperable for less than 24 hours. Also, the finding did
of centrifugal charging Pump A. An unplanned entry into Technical Specification 3.5.2,  
  not screen as potentially risk significant due to a seismic, flooding, or severe weather
Condition A, was made for approximately 10 hours. The licensee entered this issue in  
  initiating event. The inspectors identified a human performance crosscutting in the area
their corrective action program as Condition Report 21993.  
  of work practices because self-checking and communication with the supervisor failed to
The failure to follow station procedures and correctly remove the detector was a  
  prevent the event [H.4.a] (Section 1R13).
performance deficiency. The finding was more than minor because it was associated  
* Green. On November 5, 2009, inspectors identified a noncited violation of 10 CFR
with the equipment performance attribute of the Mitigating Systems Cornerstone and  
  Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure
affected the cornerstone objective to ensure the availability, reliability, and capability of  
  to perform an adequate operability evaluation required by procedure. The inspectors
systems that respond to initiating events to prevent undesirable consequences. The  
  identified that Operability Evaluation EF 09-010, Revisions 0 and 1, did not demonstrate
inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual  
  that the essential service water pumps could withstand a safe shutdown earthquake.
Chapter 0609.04, and determined that the finding was of very low safety significance  
  Revision 2 of the operability evaluation included calculations to demonstrate acceptable
(Green) because the pump was inoperable for less than 24 hours. Also, the finding did  
                                        -7-                                      Enclosure 2
not screen as potentially risk significant due to a seismic, flooding, or severe weather  
initiating event. The inspectors identified a human performance crosscutting in the area  
of work practices because self-checking and communication with the supervisor failed to  
prevent the event [H.4.a] (Section 1R13).  
*  
Green. On November 5, 2009, inspectors identified a noncited violation of 10 CFR  
Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure  
to perform an adequate operability evaluation required by procedure. The inspectors  
identified that Operability Evaluation EF 09-010, Revisions 0 and 1, did not demonstrate  
that the essential service water pumps could withstand a safe shutdown earthquake.  
Revision 2 of the operability evaluation included calculations to demonstrate acceptable  


  stresses and included pump impeller clearances. This issue is captured in the corrective
  action program as condition reports 22798 and 21572.
  The failure to perform an adequate operability evaluation per Procedures AP 28-001
- 8 -
  and AP 26C 004 was a performance deficiency. The inspectors determined that this
  finding was more than minor because it is associated with the equipment performance
  attribute of the Mitigating Systems Cornerstone, and it affected the cornerstone objective
  to ensure the availability, reliability, and capability of systems that respond to initiating
  events to prevent undesirable consequences (i.e., core damage). Specifically, this issue
Enclosure 2
  relates to the availability and reliability examples of the equipment performance attribute
stresses and included pump impeller clearances. This issue is captured in the corrective  
  because a latent common mode failure mechanism was not correctly evaluated. The
action program as condition reports 22798 and 21572.  
  inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual
The failure to perform an adequate operability evaluation per Procedures AP 28-001  
  Chapter 0609, Appendix A, and determined that the finding was of very low safety
and AP 26C 004 was a performance deficiency. The inspectors determined that this  
  significance (Green) because the issue was not a design or qualification deficiency
finding was more than minor because it is associated with the equipment performance  
  confirmed to result in loss of operability or functionality, did not represent a loss of
attribute of the Mitigating Systems Cornerstone, and it affected the cornerstone objective  
  system safety function, an actual loss of safety function of a single train for greater than
to ensure the availability, reliability, and capability of systems that respond to initiating  
  its technical specification allowed outage time, an actual loss of safety function of a
events to prevent undesirable consequences (i.e., core damage). Specifically, this issue  
  nontechnical specification risk-significant equipment train, and did not screen as
relates to the availability and reliability examples of the equipment performance attribute  
  potentially risk significant due to a seismic, flooding, or severe weather initiating event.
because a latent common mode failure mechanism was not correctly evaluated. The  
  The cause of the finding has a problem identification and resolution crosscutting aspect
inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual  
  associated with the corrective action program because Wolf Creek failed to thoroughly
Chapter 0609, Appendix A, and determined that the finding was of very low safety  
  evaluate the failure mechanism such that the resolutions address the causes and extent
significance (Green) because the issue was not a design or qualification deficiency  
  of conditions, as necessary [P.1.c] (Section 1R15).
confirmed to result in loss of operability or functionality, did not represent a loss of  
* Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a
system safety function, an actual loss of safety function of a single train for greater than  
  for failure to properly implement Procedure AP 14A-003, Scaffold Construction and
its technical specification allowed outage time, an actual loss of safety function of a  
  Use, when scaffolding was erected against operable safety-related equipment. On
nontechnical specification risk-significant equipment train, and did not screen as  
  October 15, 2009, the inspectors walked down containment and identified scaffolding in
potentially risk significant due to a seismic, flooding, or severe weather initiating event.
  contact with component cooling water piping. The tag on the scaffold explicitly stated
The cause of the finding has a problem identification and resolution crosscutting aspect  
  that it was not seismically qualified. At the time, both steam generators were inoperable
associated with the corrective action program because Wolf Creek failed to thoroughly  
  and both trains of residual heat removal were required to be operable. The inspectors
evaluate the failure mechanism such that the resolutions address the causes and extent  
  reviewed the bases for Technical Specification 3.4.7, RCS Loops - Mode 5, Loops
of conditions, as necessary [P.1.c] (Section 1R15).  
  Filled, which required an operable heat sink path from residual heat removal to
*  
  component cooling water to essential service water. This issue was entered into the
Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a  
  corrective action program as Condition Report 22464.
for failure to properly implement Procedure AP 14A-003, Scaffold Construction and  
  The construction of an unqualified scaffold against operable component cooling water
Use, when scaffolding was erected against operable safety-related equipment. On  
  piping was a performance deficiency. The inspectors determined that this finding was
October 15, 2009, the inspectors walked down containment and identified scaffolding in  
  more than minor because it is associated with the equipment performance attribute for
contact with component cooling water piping. The tag on the scaffold explicitly stated  
  the Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the
that it was not seismically qualified. At the time, both steam generators were inoperable  
  availability, reliability, and capability of systems that respond to initiating events to
and both trains of residual heat removal were required to be operable. The inspectors  
  prevent undesirable consequences (i.e., core damage). Specifically, this issue relates to
reviewed the bases for Technical Specification 3.4.7, RCS Loops - Mode 5, Loops  
  the availability and reliability examples of the equipment performance attribute because
Filled, which required an operable heat sink path from residual heat removal to  
  a latent failure mechanism was not evaluated. The inspectors evaluated the significance
component cooling water to essential service water. This issue was entered into the  
  of this finding using Inspection Manual Chapter 0609, Appendix G, Attachment 1,
corrective action program as Condition Report 22464.  
  Shutdown Operations Significance Determination Process Phase 1 Operational
The construction of an unqualified scaffold against operable component cooling water  
  Checklists for Both PWRs and BWRs. The inspectors determined that Checklist 3 was
piping was a performance deficiency. The inspectors determined that this finding was  
  applicable because the unit was in cold shutdown with the refueling cavity level less than
more than minor because it is associated with the equipment performance attribute for  
                                          -8-                                      Enclosure 2
the Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the  
availability, reliability, and capability of systems that respond to initiating events to  
prevent undesirable consequences (i.e., core damage). Specifically, this issue relates to  
the availability and reliability examples of the equipment performance attribute because  
a latent failure mechanism was not evaluated. The inspectors evaluated the significance  
of this finding using Inspection Manual Chapter 0609, Appendix G, Attachment 1,  
Shutdown Operations Significance Determination Process Phase 1 Operational  
Checklists for Both PWRs and BWRs. The inspectors determined that Checklist 3 was  
applicable because the unit was in cold shutdown with the refueling cavity level less than  


  23 feet. Using Appendix G, Attachment 1, Checklist 3, Phase 2 analysis was not
  needed and the finding was of very low safety significance (Green) because the licensee
  was able to demonstrate that the seismically unqualified scaffolding would not have
- 9 -
  resulted in a loss of safety function. The inspectors determined the cause of the finding
  had a human performance aspect in the area of resources. Specifically,
  Procedure AP 14A-003 was inadequate because it had conflicting guidance that allowed
  seismically unqualified scaffolds in Modes 5 and 6 [H.2.c] (Section 1R20).
  Cornerstone: Barrier Integrity
Enclosure 2
* Green. The inspectors identified a noncited violation of Technical Specification 3.3.1,
23 feet. Using Appendix G, Attachment 1, Checklist 3, Phase 2 analysis was not  
  Condition I, for making positive reactivity addition prohibited by technical specifications
needed and the finding was of very low safety significance (Green) because the licensee  
  in Mode 2 because one source range nuclear instrument channel was inoperable.
was able to demonstrate that the seismically unqualified scaffolding would not have  
  Following a reactor transient, one of the source range nuclear instrument channels
resulted in a loss of safety function. The inspectors determined the cause of the finding  
  experienced an unanticipated increased count rate and was declared inoperable. Wolf
had a human performance aspect in the area of resources. Specifically,  
  Creek restored the channel in an operability evaluation which cited the cause as a
Procedure AP 14A-003 was inadequate because it had conflicting guidance that allowed  
  problem in a component which was later determined not to exist in the installed
seismically unqualified scaffolds in Modes 5 and 6 [H.2.c] (Section 1R20).  
  configuration; however, the improperly restored equipment had already been used for to
Cornerstone: Barrier Integrity  
  support plant startup on August 22, 2009. Wolf Creek replaced the detector during
*  
  Refueling Outage 17. This issue was entered into the correction action program as
Green. The inspectors identified a noncited violation of Technical Specification 3.3.1,  
  Condition Report 20208.
Condition I, for making positive reactivity addition prohibited by technical specifications  
  Reactivity addition with source range channel Nuclear Instrument-31 inoperable is a
in Mode 2 because one source range nuclear instrument channel was inoperable.
  performance deficiency. The finding was more than minor because it was associated
Following a reactor transient, one of the source range nuclear instrument channels  
  with the configuration control (reactivity control) attribute of the Barrier Integrity
experienced an unanticipated increased count rate and was declared inoperable. Wolf  
  Cornerstone, and it affected the cornerstone objective to provide reasonable assurance
Creek restored the channel in an operability evaluation which cited the cause as a  
  that physical design barriers (fuel cladding, reactor coolant system, and containment)
problem in a component which was later determined not to exist in the installed  
  protect the public from radionuclide releases caused by accidents or events. The
configuration; however, the improperly restored equipment had already been used for to  
  inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual
support plant startup on August 22, 2009. Wolf Creek replaced the detector during  
  Chapter 0609.04, and determined that the finding screened to Green because the
Refueling Outage 17. This issue was entered into the correction action program as  
  finding only affected the fuel barrier. Additionally, the cause of the finding has a human
Condition Report 20208.
  performance crosscutting aspect in the area associated with the decision making.
Reactivity addition with source range channel Nuclear Instrument-31 inoperable is a  
  Specifically, Wolf Creek did not use conservative assumptions in decision making and
performance deficiency. The finding was more than minor because it was associated  
  adopt requirements to demonstrate that the proposed action is safe in order to proceed
with the configuration control (reactivity control) attribute of the Barrier Integrity  
  rather than a requirement to demonstrate that it is unsafe in order to disapprove the
Cornerstone, and it affected the cornerstone objective to provide reasonable assurance  
  action, when performing an operability evaluation for the source range Nuclear
that physical design barriers (fuel cladding, reactor coolant system, and containment)  
  Instrument 31 detector prior to restarting from a forced outage [H.1(b)] (Section 1R15).
protect the public from radionuclide releases caused by accidents or events. The  
* Green. On December 30, 2009, the inspectors identified a noncited violation of
inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual  
    Technical Specification Table 3.3.1-1, Function 18.a, when Wolf Creek restarted on
Chapter 0609.04, and determined that the finding screened to Green because the  
    May 18, 2005. During a reactor shutdown on October 7, 2006, intermediate range
finding only affected the fuel barrier. Additionally, the cause of the finding has a human  
    neutron detector Nuclear Instrument-36 did not decrease below 6E -11 amps and
performance crosscutting aspect in the area associated with the decision making.
    energize source range detector Nuclear Instrument-32. The detector was not replaced
Specifically, Wolf Creek did not use conservative assumptions in decision making and  
    until Refueling Outage 16 in March 2008. The licensee entered this issue in their
adopt requirements to demonstrate that the proposed action is safe in order to proceed  
    corrective action program as Condition Report 22450
rather than a requirement to demonstrate that it is unsafe in order to disapprove the  
  The inspectors determined that the failure to ensure that the P-6 interlock was operable
action, when performing an operability evaluation for the source range Nuclear  
  per the technical specification as defined in the bases was a performance deficiency.
Instrument 31 detector prior to restarting from a forced outage [H.1(b)] (Section 1R15).  
                                        -9-                                        Enclosure 2
*  
Green. On December 30, 2009, the inspectors identified a noncited violation of  
Technical Specification Table 3.3.1-1, Function 18.a, when Wolf Creek restarted on  
May 18, 2005. During a reactor shutdown on October 7, 2006, intermediate range  
neutron detector Nuclear Instrument-36 did not decrease below 6E -11 amps and  
energize source range detector Nuclear Instrument-32. The detector was not replaced  
until Refueling Outage 16 in March 2008. The licensee entered this issue in their  
corrective action program as Condition Report 22450  
The inspectors determined that the failure to ensure that the P-6 interlock was operable  
per the technical specification as defined in the bases was a performance deficiency.


  The finding was more than minor because it was associated with the configuration
  control (reactivity control) attribute of the Barrier Integrity Cornerstone, and it affected the
  cornerstone objective to provide reasonable assurance that physical design barriers (fuel
- 10 -
  cladding, reactor coolant system, and containment) protect the public from radionuclide
  releases caused by accidents or events. The inspectors evaluated the significance of
  this finding using Phase 1 of Inspection Manual Chapter 0609.04, and determined that
  the finding screened to Green because the P-6 interlock only affected the fuel barrier
  (Section 4OA2). This finding was not assigned a crosscutting aspect because the cause
Enclosure 2
  was not representative of current performance.
The finding was more than minor because it was associated with the configuration  
  Cornerstone: Occupational Radiation Safety
control (reactivity control) attribute of the Barrier Integrity Cornerstone, and it affected the  
* Green. The inspector identified a noncited violation of Technical Specification 5.7.2.a.1
cornerstone objective to provide reasonable assurance that physical design barriers (fuel  
  for failure to maintain administrative control of door and gate keys to high radiation areas
cladding, reactor coolant system, and containment) protect the public from radionuclide  
  with dose rates greater than 1 rem per hour but less than 500 rads per hour (referred to
releases caused by accidents or events. The inspectors evaluated the significance of  
  as locked high radiation areas). Specifically, as of October 21, 2009, the licensee did
this finding using Phase 1 of Inspection Manual Chapter 0609.04, and determined that  
  not have administrative controls over a single master key to locked high radiation areas.
the finding screened to Green because the P-6 interlock only affected the fuel barrier  
  This issue was entered into the licensees corrective action program as Condition
(Section 4OA2). This finding was not assigned a crosscutting aspect because the cause  
  Report 20973.
was not representative of current performance.  
  Failure to maintain administrative control of the master key to locked high radiation areas
Cornerstone: Occupational Radiation Safety  
  was a performance deficiency. This finding is greater than minor because if left uncorrected
*  
  the finding has the potential to lead to a more significant safety concern in that an individual
Green. The inspector identified a noncited violation of Technical Specification 5.7.2.a.1  
  could receive unanticipated radiation dose by gaining access a locked high radiation area
for failure to maintain administrative control of door and gate keys to high radiation areas  
  without the proper controls and briefing. This finding was evaluated using the occupational
with dose rates greater than 1 rem per hour but less than 500 rads per hour (referred to  
  radiation safety significance determination process and determined to be of very low safety
as locked high radiation areas). Specifically, as of October 21, 2009, the licensee did  
  significance because it did not involve: (1) as low as is reasonably achievable planning or
not have administrative controls over a single master key to locked high radiation areas.
  work control issue, (2) an overexposure, (3) a substantial potential for overexposure, or
This issue was entered into the licensees corrective action program as Condition  
  (4) an impaired ability to assess dose. Additionally, the violation has a crosscutting aspect
Report 20973.  
  in the area of human performance associated with the work practices component because
Failure to maintain administrative control of the master key to locked high radiation areas  
  the lack of peer and self-checking resulted in inadequate control of keys to locked high
was a performance deficiency. This finding is greater than minor because if left uncorrected  
  radiation areas [H.4(a)] (Section 2OS1).
the finding has the potential to lead to a more significant safety concern in that an individual  
  Cornerstone: Miscellaneous
could receive unanticipated radiation dose by gaining access a locked high radiation area  
* Severity Level IV. The inspectors identified a Severity Level IV noncited violation of
without the proper controls and briefing. This finding was evaluated using the occupational  
  10 CFR 50.73 in which the licensee failed to submit a licensee event report within 60 days
radiation safety significance determination process and determined to be of very low safety  
  following discovery of events or conditions meeting the reportability criteria. On December
significance because it did not involve: (1) as low as is reasonably achievable planning or  
  31, 2009, the inspectors identified a licensee event report that was no timely. Licensee
work control issue, (2) an overexposure, (3) a substantial potential for overexposure, or  
  Event Report 2009-009-00 was not issued within 60 days for a condition prohibited by
(4) an impaired ability to assess dose. Additionally, the violation has a crosscutting aspect  
  technical specifications, and the event report did not identify that the disabling of both trains
in the area of human performance associated with the work practices component because  
  of the P-4 interlock on August 22, 2009 was also reportable per 10 CFR 50.73(a)(2)(v). The
the lack of peer and self-checking resulted in inadequate control of keys to locked high  
  P-4 interlock was required by Technical Specification 3.3.2, function 8.a, and is discussed in
radiation areas [H.4(a)] (Section 2OS1).
  USAR, Section 7.3.8, NSSS Engineered Safety Feature Actuation System. Wolf Creek
Cornerstone: Miscellaneous  
  licensee event report 2009-009 was correct in that the interlock is not credited in accident
*  
  analysis. However, NUREG 1022, Section 3.2.6, specifies that inoperable systems required
Severity Level IV. The inspectors identified a Severity Level IV noncited violation of  
  by the technical specifications be reported, even if there are other diverse operable means
10 CFR 50.73 in which the licensee failed to submit a licensee event report within 60 days  
  of accomplishing the safety function.
following discovery of events or conditions meeting the reportability criteria. On December  
                                        - 10 -                                    Enclosure 2
31, 2009, the inspectors identified a licensee event report that was no timely. Licensee  
Event Report 2009-009-00 was not issued within 60 days for a condition prohibited by  
technical specifications, and the event report did not identify that the disabling of both trains  
of the P-4 interlock on August 22, 2009 was also reportable per 10 CFR 50.73(a)(2)(v). The  
P-4 interlock was required by Technical Specification 3.3.2, function 8.a, and is discussed in  
USAR, Section 7.3.8, NSSS Engineered Safety Feature Actuation System. Wolf Creek  
licensee event report 2009-009 was correct in that the interlock is not credited in accident  
analysis. However, NUREG 1022, Section 3.2.6, specifies that inoperable systems required  
by the technical specifications be reported, even if there are other diverse operable means  
of accomplishing the safety function.  


  The inspectors reviewed this issue in accordance with Inspection Manual Chapter 0612 and
  the NRC Enforcement Manual. Through this review, the inspectors determined that
  traditional enforcement was applicable to this issue because the NRC's regulatory ability
- 11 -
  was affected. Specifically, the NRC relies on the licensee to identify and report conditions or
  events meeting the criteria specified in regulations in order to perform its regulatory function,
  and when this is not done, the regulatory function is impacted. The inspectors determined
  that this finding was not suitable for evaluation using the significance determination process,
  and as such, was evaluated in accordance with the NRC Enforcement Policy. The finding
Enclosure 2
  was reviewed by NRC management, and because the violation was determined to be of
The inspectors reviewed this issue in accordance with Inspection Manual Chapter 0612 and  
  very low safety significance, was not repetitive or willful, and was entered into the corrective
the NRC Enforcement Manual. Through this review, the inspectors determined that  
  action program, this violation is being treated as a Severity Level IV noncited violation
traditional enforcement was applicable to this issue because the NRC's regulatory ability  
  consistent with the NRC Enforcement Policy. This finding was determined to have a
was affected. Specifically, the NRC relies on the licensee to identify and report conditions or  
  crosscutting aspect in the area of problem identification and resolution associated with the
events meeting the criteria specified in regulations in order to perform its regulatory function,  
  corrective action program in that the licensee failed to appropriately and thoroughly evaluate
and when this is not done, the regulatory function is impacted. The inspectors determined  
  for reportability aspects all factors and time frames associated with the inoperability of the
that this finding was not suitable for evaluation using the significance determination process,  
  engineered safety features actuation system [P.1(c)] (Section 4OA3).
and as such, was evaluated in accordance with the NRC Enforcement Policy. The finding  
B. Licensee-Identified Violations
was reviewed by NRC management, and because the violation was determined to be of  
  Two violations of very low safety significance, which were identified by the licensee,
very low safety significance, was not repetitive or willful, and was entered into the corrective  
  have been reviewed by the inspectors. Corrective actions taken or planned by the
action program, this violation is being treated as a Severity Level IV noncited violation  
  licensee have been entered into the licensees corrective action program. These
consistent with the NRC Enforcement Policy. This finding was determined to have a  
  violations and corrective action tracking numbers (condition report numbers) are listed in
crosscutting aspect in the area of problem identification and resolution associated with the  
  Section 4OA7.
corrective action program in that the licensee failed to appropriately and thoroughly evaluate  
                                        - 11 -                                  Enclosure 2
for reportability aspects all factors and time frames associated with the inoperability of the  
engineered safety features actuation system [P.1(c)] (Section 4OA3).  
B.  
Licensee-Identified Violations  
Two violations of very low safety significance, which were identified by the licensee,  
have been reviewed by the inspectors. Corrective actions taken or planned by the  
licensee have been entered into the licensees corrective action program. These  
violations and corrective action tracking numbers (condition report numbers) are listed in  
Section 4OA7.  


                                          REPORT DETAILS
                                    Summary of Plant Status
The plant started the inspection period at 100 percent rated thermal power. On October 10,
- 12 -
2009, Wolf Creek shutdown for Refueling Outage 17. On November 17, 2009, Wolf Creek
achieved criticality and on November 24, 2009, Wolf Creek achieved 100 percent power and
remained there for the remainder of the inspection period.
1.     REACTOR SAFETY
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency
Enclosure 2
      Preparedness
REPORT DETAILS  
1R01 Adverse Weather Protection (71111.01)
Summary of Plant Status  
.1     Readiness to Cope with External Flooding
The plant started the inspection period at 100 percent rated thermal power. On October 10,  
  a. Inspection Scope
2009, Wolf Creek shutdown for Refueling Outage 17. On November 17, 2009, Wolf Creek  
        On October 28, 2009, the inspectors evaluated the design, material condition, and
achieved criticality and on November 24, 2009, Wolf Creek achieved 100 percent power and  
        procedures for coping with the design basis probable maximum flood. The evaluation
remained there for the remainder of the inspection period.  
        included a review to check for deviations from the descriptions provided in the Updated
1.  
        Safety Analysis Report (USAR) for features intended to mitigate the potential for
REACTOR SAFETY  
        flooding from external factors. As part of this evaluation, the inspectors checked for
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency  
        obstructions that could prevent draining, checked that the roofs did not contain obvious
Preparedness  
        loose items that could clog drains in the event of heavy precipitation, and determined
1R01 Adverse Weather Protection (71111.01)  
        that barriers required to mitigate the flood were in place and operable. Additionally, the
.1  
        inspectors performed a walkdown of the protected area to identify any modification to
Readiness to Cope with External Flooding  
        the site that would inhibit site drainage during a probable maximum precipitation event
        or allow water ingress past a barrier. The inspectors also reviewed the abnormal
a.  
        operating procedure for mitigating the design basis flood to ensure it could be
Inspection Scope  
        implemented as written.
        These activities constitute completion of one external flooding sample as defined in
On October 28, 2009, the inspectors evaluated the design, material condition, and  
        Inspection Procedure IP 71111.01-05.
procedures for coping with the design basis probable maximum flood. The evaluation  
  b.  Findings
included a review to check for deviations from the descriptions provided in the Updated  
      No findings of significance were identified.
Safety Analysis Report (USAR) for features intended to mitigate the potential for  
                                            - 12 -                                Enclosure 2
flooding from external factors. As part of this evaluation, the inspectors checked for  
obstructions that could prevent draining, checked that the roofs did not contain obvious  
loose items that could clog drains in the event of heavy precipitation, and determined  
that barriers required to mitigate the flood were in place and operable. Additionally, the  
inspectors performed a walkdown of the protected area to identify any modification to  
the site that would inhibit site drainage during a probable maximum precipitation event  
or allow water ingress past a barrier. The inspectors also reviewed the abnormal  
operating procedure for mitigating the design basis flood to ensure it could be  
implemented as written.  
These activities constitute completion of one external flooding sample as defined in  
Inspection Procedure IP 71111.01-05.  
b.  
Findings
   
No findings of significance were identified.  


1R04 Equipment Alignments (71111.04)
.1   Partial Walkdown
  a. Inspection Scope
- 13 -
      The inspectors performed partial walkdown of the following risk-significant systems:
      *       October 21, 2009, Train A while emergency diesel generator B and offsite power
              out of service for maintenance
      *       October 21, 2009, Spent fuel pool train A while spent fuel pool train B out of
              service
Enclosure 2
      The inspectors selected these systems based on their risk significance relative to the
1R04 Equipment Alignments (71111.04)
      Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
.1  
      to identify any discrepancies that could affect the function of the system, and, therefore,
Partial Walkdown  
      potentially increase risk. The inspectors reviewed applicable operating Procedures,
a.  
      system diagrams, USAR, technical specification requirements, administrative technical
Inspection Scope  
      specifications, outstanding work orders, condition reports, and the impact of ongoing
The inspectors performed partial walkdown of the following risk-significant systems:  
      work activities on redundant trains of equipment in order to identify conditions that could
*  
      have rendered the systems incapable of performing their intended functions. The
October 21, 2009, Train A while emergency diesel generator B and offsite power  
      inspectors also walked down accessible portions of the systems to verify system
out of service for maintenance  
      components and support equipment were aligned correctly and operable. The
*  
      inspectors examined the material condition of the components and observed operating
October 21, 2009, Spent fuel pool train A while spent fuel pool train B out of  
      parameters of equipment to verify that there were no obvious deficiencies. The
service  
      inspectors also verified that the licensee had properly identified and resolved equipment
The inspectors selected these systems based on their risk significance relative to the  
      alignment problems that could cause initiating events or impact the capability of
Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted  
      mitigating systems or barriers and entered them into the corrective action program with
to identify any discrepancies that could affect the function of the system, and, therefore,  
      the appropriate significance characterization. Specific documents reviewed during this
potentially increase risk. The inspectors reviewed applicable operating Procedures,  
      inspection are listed in the attachment.
system diagrams, USAR, technical specification requirements, administrative technical  
      These activities constitute completion of two partial system walkdown samples as
specifications, outstanding work orders, condition reports, and the impact of ongoing  
      defined in Inspection Procedure IP 71111.04-05.
work activities on redundant trains of equipment in order to identify conditions that could  
  b. Findings
have rendered the systems incapable of performing their intended functions. The  
      No findings of significance were identified.
inspectors also walked down accessible portions of the systems to verify system  
1R05 Fire Protection (71111.05)
components and support equipment were aligned correctly and operable. The  
.1   Quarterly Fire Inspection Tours
inspectors examined the material condition of the components and observed operating  
  a. Inspection Scope
parameters of equipment to verify that there were no obvious deficiencies. The  
      The inspectors conducted fire protection walkdowns that were focused on availability,
inspectors also verified that the licensee had properly identified and resolved equipment  
      accessibility, and the condition of firefighting equipment in the following risk-significant
alignment problems that could cause initiating events or impact the capability of  
      plant areas:
mitigating systems or barriers and entered them into the corrective action program with  
                                          - 13 -                                    Enclosure 2
the appropriate significance characterization. Specific documents reviewed during this  
inspection are listed in the attachment.  
These activities constitute completion of two partial system walkdown samples as  
defined in Inspection Procedure IP 71111.04-05.  
b.  
Findings  
No findings of significance were identified.  
1R05 Fire Protection (71111.05)  
.1  
Quarterly Fire Inspection Tours  
a.  
Inspection Scope  
The inspectors conducted fire protection walkdowns that were focused on availability,  
accessibility, and the condition of firefighting equipment in the following risk-significant  
plant areas:  


      *       October 7, 2009, Auxiliary boiler oil combustion Impact on turbine-driven auxiliary
              feedwater room
      *       October 29, 2009, Spent fuel pool Room A
- 14 -
      *       October 15, 2009, All levels of containment in Mode 5
      *       November 12, 2009, Refueling water storage tank valve house
      The inspectors reviewed areas to assess if licensee personnel had implemented a fire
      protection program that adequately controlled combustibles and ignition sources within
      the plant; effectively maintained fire detection and suppression capability; maintained
Enclosure 2
      passive fire protection features in good material condition; and had implemented
*  
      adequate compensatory measures for out of service, degraded or inoperable fire
October 7, 2009, Auxiliary boiler oil combustion Impact on turbine-driven auxiliary  
      protection equipment, systems, or features, in accordance with the licensees fire plan.
feedwater room
      The inspectors selected fire areas based on their overall contribution to internal fire risk
*  
      as documented in the plants individual plant examination of external events with later
October 29, 2009, Spent fuel pool Room A
      additional insights, their potential to affect equipment that could initiate or mitigate a
*  
      plant transient, or their impact on the plants ability to respond to a security event. Using
October 15, 2009, All levels of containment in Mode 5  
      the documents listed in the attachment, the inspectors verified that fire hoses and
*  
      extinguishers were in their designated locations and available for immediate use; that
November 12, 2009, Refueling water storage tank valve house  
      fire detectors and sprinklers were unobstructed, that transient material loading was
The inspectors reviewed areas to assess if licensee personnel had implemented a fire  
      within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
protection program that adequately controlled combustibles and ignition sources within  
      be in satisfactory condition. The inspectors also verified that minor issues identified
the plant; effectively maintained fire detection and suppression capability; maintained  
      during the inspection were entered into the licensees corrective action program.
passive fire protection features in good material condition; and had implemented  
      Specific documents reviewed during this inspection are listed in the attachment.
adequate compensatory measures for out of service, degraded or inoperable fire  
      These activities constitute completion of four quarterly fire-protection inspection samples
protection equipment, systems, or features, in accordance with the licensees fire plan.
      as defined by Inspection Procedure IP 71111.05-05.
The inspectors selected fire areas based on their overall contribution to internal fire risk  
  b. Findings
as documented in the plants individual plant examination of external events with later  
.1   Failure to Correct Discolored Boric Acid Deposits
additional insights, their potential to affect equipment that could initiate or mitigate a  
      Introduction. The inspectors identified a Green cited violation of 10 CFR Part 50,
plant transient, or their impact on the plants ability to respond to a security event. Using  
      Appendix B, Criterion XVI, Corrective Action, for the failure to take action to stop
the documents listed in the attachment, the inspectors verified that fire hoses and  
      leakage from the base of the refueling water storage tank or evaluate the leakage and
extinguishers were in their designated locations and available for immediate use; that  
      wastage for acceptability.
fire detectors and sprinklers were unobstructed, that transient material loading was  
      Description. During the component design basis inspection in June 2007, the inspection
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to  
      team noted white and brown deposits resembling boric acid at the base of the refueling
be in satisfactory condition. The inspectors also verified that minor issues identified  
      water storage tank. The licensee informed the team that past analysis had determined
during the inspection were entered into the licensees corrective action program.
      these deposits were from calcium-silicate insulation which had been used for insulating
Specific documents reviewed during this inspection are listed in the attachment.  
      the refueling water storage tank. In 1998, the licensee had initiated Problem
These activities constitute completion of four quarterly fire-protection inspection samples  
      Identification Request 1998-3860 to pursue the nature of the deposits and discovered
as defined by Inspection Procedure IP 71111.05-05.  
      that the deposits did contain amounts of insulation, but also contained boron. The
b.  
      licensee had dismissed the boron as spillage from a sampling evolution. On two
Findings  
      subsequent occasions after 1998, the deposits were questioned by the licensee and
.1  
                                            - 14 -                                    Enclosure 2
Failure to Correct Discolored Boric Acid Deposits  
Introduction. The inspectors identified a Green cited violation of 10 CFR Part 50,  
Appendix B, Criterion XVI, Corrective Action, for the failure to take action to stop  
leakage from the base of the refueling water storage tank or evaluate the leakage and  
wastage for acceptability.  
Description. During the component design basis inspection in June 2007, the inspection  
team noted white and brown deposits resembling boric acid at the base of the refueling  
water storage tank. The licensee informed the team that past analysis had determined  
these deposits were from calcium-silicate insulation which had been used for insulating  
the refueling water storage tank. In 1998, the licensee had initiated Problem  
Identification Request 1998-3860 to pursue the nature of the deposits and discovered  
that the deposits did contain amounts of insulation, but also contained boron. The  
licensee had dismissed the boron as spillage from a sampling evolution. On two  
subsequent occasions after 1998, the deposits were questioned by the licensee and  


again dismissed as insulation based on the 1998 resolution. In each of these cases the
deposits were cleaned up, and the problem identification requests written only
addressed the poor materiel condition of the area. The component design basis
- 15 -
inspection team questioned the previous conclusions that the deposits were insulation
material based on the strong resemblance to boric acid deposits from leakage of reactor
coolant from the refueling water storage tank. The licensee sent samples of the deposits
for offsite laboratory analysis, which confirmed that the deposits contained boron.
Subsequently, the licensee performed inspections of the carbon steel components in the
Enclosure 2
area and determined that no significant wastage had occurred and operability of the
again dismissed as insulation based on the 1998 resolution. In each of these cases the  
refueling water storage tank and its surrounding components was not affected. The
deposits were cleaned up, and the problem identification requests written only  
inspection team documented a noncited violation of 10 CFR Part 50, Appendix B,
addressed the poor materiel condition of the area. The component design basis  
Criterion XVI, for inadequate corrective actions in response to the leakage from the
inspection team questioned the previous conclusions that the deposits were insulation  
refueling water storage tank, documented in NRC Inspection Report 05000482/2007006
material based on the strong resemblance to boric acid deposits from leakage of reactor  
(ADAMS ML072880678)
coolant from the refueling water storage tank. The licensee sent samples of the deposits  
On November 12, 2009, the resident inspectors walked down the refueling water storage
for offsite laboratory analysis, which confirmed that the deposits contained boron.
tank valve house and again identified that the base of the refueling water storage tank
Subsequently, the licensee performed inspections of the carbon steel components in the  
had deposits that resembled boric acid in several locations. Some deposits had
area and determined that no significant wastage had occurred and operability of the  
progressed up the tank bolting several inches from the floor. Initially, Wolf Creek again
refueling water storage tank and its surrounding components was not affected. The  
maintained that the deposits were calcium silicate from insulation. The inspectors
inspection team documented a noncited violation of 10 CFR Part 50, Appendix B,  
questioned the licensee about the deposits, and laboratory testing again demonstrated
Criterion XVI, for inadequate corrective actions in response to the leakage from the  
the presence of boric acid.
refueling water storage tank, documented in NRC Inspection Report 05000482/2007006  
The inspectors reviewed the actions Wolf Creek had taken in response to NCV
(ADAMS ML072880678)  
05000482/2007006-03 in the component design basis inspection report. Wolf Creek had
On November 12, 2009, the resident inspectors walked down the refueling water storage  
performed a boric acid corrosion evaluation as part of Work Order 07-300734-000, which
tank valve house and again identified that the base of the refueling water storage tank  
concluded that the refueling water storage tank leak was not active, though the tank
had deposits that resembled boric acid in several locations. Some deposits had  
deposits reappeared after cleanings in July 2007, August 2008, March 2009, June 2009,
progressed up the tank bolting several inches from the floor. Initially, Wolf Creek again  
and September 2009. Wolf Creek attempted to repair roof leaks in the refueling water
maintained that the deposits were calcium silicate from insulation. The inspectors  
storage tank valve house as a source of rain water ingress, but took no action to address
questioned the licensee about the deposits, and laboratory testing again demonstrated  
the source of the boric acid in the deposits. Wolf Creek took several samples of
the presence of boric acid.  
deposits from the base of the refueling tank. Though one sample in June 2009 did not
The inspectors reviewed the actions Wolf Creek had taken in response to NCV  
contain boric acid, the majority of samples, including the most recent sample from
05000482/2007006-03 in the component design basis inspection report. Wolf Creek had  
November 2009, did contain boron, indicating that leakage from the base of the refueling
performed a boric acid corrosion evaluation as part of Work Order 07-300734-000, which  
water storage tank continued to exist. The inspectors concluded that Wolf Creek had
concluded that the refueling water storage tank leak was not active, though the tank  
failed to restore compliance from the noncited violation involving the failure to correct
deposits reappeared after cleanings in July 2007, August 2008, March 2009, June 2009,  
refueling water storage tank leakage in the component design basis inspection report.
and September 2009. Wolf Creek attempted to repair roof leaks in the refueling water  
Analysis. The failure to implement corrective actions for the refueling water storage tank
storage tank valve house as a source of rain water ingress, but took no action to address  
leakage was a performance deficiency. Traditional enforcement does not apply since
the source of the boric acid in the deposits. Wolf Creek took several samples of  
there were no actual safety consequences or potential for impacting the NRC's
deposits from the base of the refueling tank. Though one sample in June 2009 did not  
regulatory function, and the finding was not the result of any willful violation of NRC
contain boric acid, the majority of samples, including the most recent sample from  
requirements or Wolf Creek procedures. The issue was greater than minor because if
November 2009, did contain boron, indicating that leakage from the base of the refueling  
left uncorrected, the failure to correct the presence of boric acid for extended periods of
water storage tank continued to exist. The inspectors concluded that Wolf Creek had  
time would become a more significant-safety concern, in that, continued wastage could
failed to restore compliance from the noncited violation involving the failure to correct  
impact the studs and tank operability. The finding affected the Mitigating Systems
refueling water storage tank leakage in the component design basis inspection report.  
Cornerstone, using the Phase 1 worksheets in Inspection Manual Chapter 0609.04,
Analysis. The failure to implement corrective actions for the refueling water storage tank  
"Significance Determination Process." The inspectors determined that the finding had
leakage was a performance deficiency. Traditional enforcement does not apply since  
                                    - 15 -                                    Enclosure 2
there were no actual safety consequences or potential for impacting the NRC's  
regulatory function, and the finding was not the result of any willful violation of NRC  
requirements or Wolf Creek procedures. The issue was greater than minor because if  
left uncorrected, the failure to correct the presence of boric acid for extended periods of  
time would become a more significant-safety concern, in that, continued wastage could  
impact the studs and tank operability. The finding affected the Mitigating Systems  
Cornerstone, using the Phase 1 worksheets in Inspection Manual Chapter 0609.04,  
"Significance Determination Process." The inspectors determined that the finding had  


  very low safety significance (Green) because it did not result in a system or component
  being inoperable and it did not screen as potentially risk significant due to a seismic,
  flooding, or severe weather initiating event. The inspectors identified a crosscutting
- 16 -
  aspect in the area of human performance associated with resources. Specifically, Wolf
  Creek did not maintain long-term plant safety minimizing corrective maintenance
  deferrals and this long-standing equipment issue [H.2(c)].
  Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,
  requires, in part, that measures shall be established to assure that conditions adverse to
Enclosure 2
  quality are promptly identified and corrected. Contrary to the above, from 1998 to
very low safety significance (Green) because it did not result in a system or component  
  December 31, 2009, Wolf Creek did not correct the condition adverse to quality.
being inoperable and it did not screen as potentially risk significant due to a seismic,  
  Specifically, Wolf Creek did not take action to correct leakage from the refueling water
flooding, or severe weather initiating event. The inspectors identified a crosscutting  
  storage tank. This issue and the corrective actions are being tracked in Condition
aspect in the area of human performance associated with resources. Specifically, Wolf  
  Reports 2007-02742 and 22866. Due to the licensees failure to restore compliance
Creek did not maintain long-term plant safety minimizing corrective maintenance  
  from previous NCV 05000482/2007006-03 within a reasonable time after the violation
deferrals and this long-standing equipment issue [H.2(c)].  
  was identified, this violation is being cited as a Notice of Violation consistent with Section
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,  
  VI.A of the Enforcement Policy: VIO 05000482/2009005-01, Failure to Correct
requires, in part, that measures shall be established to assure that conditions adverse to  
  Discolored Boric Acid Deposits (EA-10-004).
quality are promptly identified and corrected. Contrary to the above, from 1998 to  
.2 Control of Transient Ignition Sources
December 31, 2009, Wolf Creek did not correct the condition adverse to quality.
  Introduction. The inspectors identified a noncited violation of Technical
Specifically, Wolf Creek did not take action to correct leakage from the refueling water  
  Specification 5.4.1.a for an inadequate procedure for control of transient ignition sources
storage tank. This issue and the corrective actions are being tracked in Condition  
  due to exempting the use of flapper wheels from the requirements of AP 10-101,
Reports 2007-02742 and 22866. Due to the licensees failure to restore compliance  
  Control of Transient Ignition Sources.
from previous NCV 05000482/2007006-03 within a reasonable time after the violation  
  Description. On October 21, 2009, NRC inspectors observed maintenance personnel
was identified, this violation is being cited as a Notice of Violation consistent with Section  
  performing weld preparation work on essential service water piping to containment
VI.A of the Enforcement Policy: VIO 05000482/2009005-01, Failure to Correct  
  cooler B. The inspectors observed that the ignition control barriers for the hot work were
Discolored Boric Acid Deposits (EA-10-004).  
  insufficient, in that the sparks from the preparation work extended four to five feet from
.2  
  the job site and there was no fire watch apparent. When the inspectors questioned the
Control of Transient Ignition Sources  
  maintenance personnel regarding the posting of a fire watch, the maintenance personnel
Introduction. The inspectors identified a noncited violation of Technical  
  stated that they were using a flapper wheel and a fire watch was not required.
Specification 5.4.1.a for an inadequate procedure for control of transient ignition sources  
  On December 4, 2003, the licensee modified Procedure AP-10-101, Control of
due to exempting the use of flapper wheels from the requirements of AP 10-101,  
  Transient Ignition Sources, such that the use of flapper wheels was exempted from the
Control of Transient Ignition Sources.  
  requirements of Procedure AP10-101. The inspectors determined that the revised
  procedure adversely affected the fire safety in the affected area. This was based on
Description. On October 21, 2009, NRC inspectors observed maintenance personnel  
  recognition that the ability of the fire watch was not limited to fire identification in a timely
performing weld preparation work on essential service water piping to containment  
  manner, but also on mitigation actions that an established fire watch could take in the
cooler B. The inspectors observed that the ignition control barriers for the hot work were  
  event of fires. These could include such actions as the ability to close doors limiting fire
insufficient, in that the sparks from the preparation work extended four to five feet from  
  exposure to adjacent areas and providing more timely fire detection capability in certain
the job site and there was no fire watch apparent. When the inspectors questioned the  
  cases. The inspectors concluded that the licensee inappropriately revised the procedure
maintenance personnel regarding the posting of a fire watch, the maintenance personnel  
  to exempt the use of all flapper wheels without posting a fire watch. The inspectors
stated that they were using a flapper wheel and a fire watch was not required.  
  determined that the inadequate procedure increased the risk of fires in the plant.
  Analysis. The licensee's failure to provide an adequate procedure to control transient
On December 4, 2003, the licensee modified Procedure AP-10-101, Control of  
  ignition sources was a performance deficiency and was reasonably within the ability of
Transient Ignition Sources, such that the use of flapper wheels was exempted from the  
                                          - 16 -                                    Enclosure 2
requirements of Procedure AP10-101. The inspectors determined that the revised  
procedure adversely affected the fire safety in the affected area. This was based on  
recognition that the ability of the fire watch was not limited to fire identification in a timely  
manner, but also on mitigation actions that an established fire watch could take in the  
event of fires. These could include such actions as the ability to close doors limiting fire  
exposure to adjacent areas and providing more timely fire detection capability in certain  
cases. The inspectors concluded that the licensee inappropriately revised the procedure  
to exempt the use of all flapper wheels without posting a fire watch. The inspectors  
determined that the inadequate procedure increased the risk of fires in the plant.  
Analysis. The licensee's failure to provide an adequate procedure to control transient  
ignition sources was a performance deficiency and was reasonably within the ability of  


    the licensee to prevent. The inspectors concluded that this issue had a realistic
    likelihood of affecting safety. Failure to properly evaluate the removal of the fire watch
    posting requirements could adversely affect or degrade the ability of the licensee to
- 17 -
    identify and report fires caused by hot work, in a timely manner. Specifically, the use of
    nonconservative exemptions for requiring fire watches to be posted could affect the
    ability to adequately reduce the risk of fires in the plant. This finding is more than minor
    because it affected the Mitigating Systems Cornerstone attribute of Protection Against
    External Factors - Fires, and adversely affected the cornerstone objective to ensure the
Enclosure 2
    availability, reliability, and capability of systems that respond to initiating events to
the licensee to prevent. The inspectors concluded that this issue had a realistic  
    prevent undesirable consequences. The lack of a posted fire watch could adversely
likelihood of affecting safety. Failure to properly evaluate the removal of the fire watch  
    affect the ability to achieve and maintain safe shutdown in the event of a severe fire in
posting requirements could adversely affect or degrade the ability of the licensee to  
    the affected area. Inspection Manual Chapter 0609, Appendix F, Fire Protection
identify and report fires caused by hot work, in a timely manner. Specifically, the use of  
    Significance Determination Process, could not be used to effectively evaluate the
nonconservative exemptions for requiring fire watches to be posted could affect the  
    finding in relation to defense-in-depth strategies because it had potential effects across
ability to adequately reduce the risk of fires in the plant. This finding is more than minor  
    multiple areas and conditions. Therefore, in accordance with Inspection Manual
because it affected the Mitigating Systems Cornerstone attribute of Protection Against  
    Chapter 0609, Appendix M, the safety significance was determined by regional
External Factors - Fires, and adversely affected the cornerstone objective to ensure the  
    management review and concluded that the finding was of very low safety significance
availability, reliability, and capability of systems that respond to initiating events to  
    (Green) since there were no combustibles in the immediate area and fire extinguishers
prevent undesirable consequences. The lack of a posted fire watch could adversely  
    were readily available. The capability of other principal defense-in-depth fire protection
affect the ability to achieve and maintain safe shutdown in the event of a severe fire in  
    features were unaffected, such as the associated fire barriers, control of transient
the affected area. Inspection Manual Chapter 0609, Appendix F, Fire Protection  
    combustibles, manual fire suppression equipment, and the fire brigade. Additionally, the
Significance Determination Process, could not be used to effectively evaluate the  
    finding was not associated with a qualification deficiency, did not result in a loss of safety
finding in relation to defense-in-depth strategies because it had potential effects across  
    function for a system, and was not risk significance due to external initiating events.
multiple areas and conditions. Therefore, in accordance with Inspection Manual  
    Enforcement. Technical Specification 5.4.1.a requires, in part, that written procedures
Chapter 0609, Appendix M, the safety significance was determined by regional  
    shall be established and maintained covering the applicable procedures recommended
management review and concluded that the finding was of very low safety significance  
    in Regulatory Guide 1.33, Revision 2, Appendix A, February 1972. Regulatory
(Green) since there were no combustibles in the immediate area and fire extinguishers  
    Guide 1.33, "Quality Assurance Program Requirements (Operation)," Revision 2,
were readily available. The capability of other principal defense-in-depth fire protection  
    Appendix A, Section 1.l, requires that procedures be written for plant fire protection
features were unaffected, such as the associated fire barriers, control of transient  
    program. Contrary to this requirement, from December 4, 2003, until October 21, 2009,
combustibles, manual fire suppression equipment, and the fire brigade. Additionally, the  
    the licensee inappropriately exempted the use of flapper wheels from the requirements
finding was not associated with a qualification deficiency, did not result in a loss of safety  
    of Procedure AP 10-101, Control of Transient Ignition Sources, reducing the fire safety
function for a system, and was not risk significance due to external initiating events.
    of the plant. Because this issue was determined to be of very low safety significance
    (Green) and was entered into the licensees corrective action program as Condition
Enforcement. Technical Specification 5.4.1.a requires, in part, that written procedures  
    Report AR 00020993, this violation is being treated as a noncited violation in accordance
shall be established and maintained covering the applicable procedures recommended  
    with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2009005-02,
in Regulatory Guide 1.33, Revision 2, Appendix A, February 1972. Regulatory  
    Control of Transient Ignition Sources.
Guide 1.33, "Quality Assurance Program Requirements (Operation)," Revision 2,  
1R06 Flood Protection Measures (71111.06)
Appendix A, Section 1.l, requires that procedures be written for plant fire protection  
  a. Inspection Scope
program. Contrary to this requirement, from December 4, 2003, until October 21, 2009,  
    The inspectors reviewed the USAR, the flooding analysis, and plant procedures to
the licensee inappropriately exempted the use of flapper wheels from the requirements  
    assess seasonal susceptibilities involving internal flooding; reviewed the USAR and
of Procedure AP 10-101, Control of Transient Ignition Sources, reducing the fire safety  
    corrective action program to determine if licensee personnel identified and corrected
of the plant. Because this issue was determined to be of very low safety significance  
    flooding problems; inspected underground bunkers/manholes to verify the adequacy of
(Green) and was entered into the licensees corrective action program as Condition  
    sump pumps, level alarm circuits, cable splices subject to submergence, and drainage
Report AR 00020993, this violation is being treated as a noncited violation in accordance  
                                            - 17 -                                    Enclosure 2
with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2009005-02,  
Control of Transient Ignition Sources.  
1R06 Flood Protection Measures (71111.06)  
a.  
Inspection Scope  
The inspectors reviewed the USAR, the flooding analysis, and plant procedures to  
assess seasonal susceptibilities involving internal flooding; reviewed the USAR and  
corrective action program to determine if licensee personnel identified and corrected  
flooding problems; inspected underground bunkers/manholes to verify the adequacy of  
sump pumps, level alarm circuits, cable splices subject to submergence, and drainage  


      for bunkers/manholes; verified that operator actions for coping with flooding can
      reasonably achieve the desired outcomes; and walked down the area listed below to
      verify the adequacy of equipment seals located below the flood line, floor and wall
- 18 -
      penetration seals, watertight door seals, common drain lines and sumps, sump pumps,
      level alarms, and control circuits, and temporary or removable flood barriers. Specific
      documents reviewed during this inspection are listed in the attachment.
      *       October 6, 2009, Auxiliary feedwater rooms and sump pumps
      These activities constitute completion of one flood protection measures inspection
Enclosure 2
      sample as defined by Inspection Procedure IP 71111.06-05.
for bunkers/manholes; verified that operator actions for coping with flooding can  
  b. Findings
reasonably achieve the desired outcomes; and walked down the area listed below to  
      No findings of significance were identified.
verify the adequacy of equipment seals located below the flood line, floor and wall  
1R07 Heat Sink Performance (71111.07)
penetration seals, watertight door seals, common drain lines and sumps, sump pumps,  
.1   Annual Inspection
level alarms, and control circuits, and temporary or removable flood barriers. Specific  
  a. Inspection Scope
documents reviewed during this inspection are listed in the attachment.
      The inspectors reviewed licensee programs, verified performance against industry
*  
      standards, and reviewed critical operating parameters and maintenance records.
October 6, 2009, Auxiliary feedwater rooms and sump pumps  
      *       January 14, 2009, STN PE-38 on containment cooler SGN01D
These activities constitute completion of one flood protection measures inspection  
      The inspectors verified that performance tests were satisfactorily conducted for heat
sample as defined by Inspection Procedure IP 71111.06-05.  
      exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the
b.  
      periodic maintenance method outlined in Electric Power Research Institute
Findings  
      Report NP 7552, "Heat Exchanger Performance Monitoring Guidelines;" the licensee
No findings of significance were identified.  
      properly utilized biofouling controls; the licensees heat exchanger inspections
1R07 Heat Sink Performance (71111.07)  
      adequately assessed the state of cleanliness of their tubes; and the heat exchanger was
.1  
      correctly categorized under 10 CFR 50.65, Requirements for Monitoring the
Annual Inspection  
      Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed
a.  
      during this inspection are listed in the attachment.
Inspection Scope  
      These activities constitute completion of one heat sink inspection sample as defined by
The inspectors reviewed licensee programs, verified performance against industry  
      Inspection Procedure IP 71111.07-05.
standards, and reviewed critical operating parameters and maintenance records.
  b. Findings
*  
      No findings of significance were identified.
January 14, 2009, STN PE-38 on containment cooler SGN01D  
                                          - 18 -                                  Enclosure 2
The inspectors verified that performance tests were satisfactorily conducted for heat  
exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the  
periodic maintenance method outlined in Electric Power Research Institute  
Report NP 7552, "Heat Exchanger Performance Monitoring Guidelines;" the licensee  
properly utilized biofouling controls; the licensees heat exchanger inspections  
adequately assessed the state of cleanliness of their tubes; and the heat exchanger was  
correctly categorized under 10 CFR 50.65, Requirements for Monitoring the  
Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed  
during this inspection are listed in the attachment.  
These activities constitute completion of one heat sink inspection sample as defined by  
Inspection Procedure IP 71111.07-05.  
b.  
Findings  
No findings of significance were identified.  


1R08 Inservice Inspection Activities (71111.08)
.1   Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water
      Reactor Vessel Upper Head Penetration Inspections, Boric Acid Corrosion Control
- 19 -
      (71111.08-02.01)
  a. Inspection Scope
      The inspection procedure requires review of two or three types of nondestructive
      examination activities and, if performed, one to three welds on the reactor coolant
      system pressure boundary. It also requires review of one or two examinations with
Enclosure 2
      relevant indications (if any were found) that have been accepted by the licensee for
1R08 Inservice Inspection Activities (71111.08)  
      continued service.
      The inspectors directly observed the following nondestructive examinations:
.1  
              SYSTEM                       WELD IDENTIFICATION             EXAMINATION
Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water  
                                                                                TYPE
Reactor Vessel Upper Head Penetration Inspections, Boric Acid Corrosion Control  
      Feedwater System           Check Valve. Root pass indication             MT
(71111.08-02.01)
                                  repair. Area 5, West Bay
                                  Drawing WIP-M-13AE05-012-A-1
a.
                                  WO 08-305300-049
Inspection Scope  
      Charging Pump               Vent valve. 1974 foot elevation               PT
      Room B                      auxiliary building, Room 1108
The inspection procedure requires review of two or three types of nondestructive  
                                  Drawing WIP-M-13BG02-006-A-1
examination activities and, if performed, one to three welds on the reactor coolant  
                                  WO 08-310289-043
system pressure boundary. It also requires review of one or two examinations with  
      Safety Injection           Vent Valve. Located in safety                 PT
relevant indications (if any were found) that have been accepted by the licensee for  
                                  injection pump Room A
continued service.  
                                  Drawing WIP-M-13EM01-008-A-1
                                  WO 0-310289-077
The inspectors directly observed the following nondestructive examinations:  
      Chemical and Volume         Blowdown line coupling letdown heat           PT
SYSTEM  
      Control System              exchanger room Drawing M-13BG34
WELD IDENTIFICATION  
                                  WO 06-288993-000
EXAMINATION
      Feedwater System           Check valve hinge pin seal weld.               PT
TYPE  
                                  2047 foot elevation, RB C loop
Feedwater System  
                                  Drawing WOP-M-13AE04-008-A-1
Check Valve. Root pass indication  
                                  WO 08-305300-013
repair. Area 5, West Bay  
                                          - 19 -                                Enclosure 2
Drawing WIP-M-13AE05-012-A-1  
WO 08-305300-049  
MT
Charging Pump
Room B
Vent valve. 1974 foot elevation  
auxiliary building, Room 1108  
Drawing WIP-M-13BG02-006-A-1  
WO 08-310289-043  
PT
Safety Injection  
Vent Valve. Located in safety  
injection pump Room A  
Drawing WIP-M-13EM01-008-A-1  
WO 0-310289-077  
PT
Chemical and Volume  
Control System 
Blowdown line coupling letdown heat  
exchanger room Drawing M-13BG34  
WO 06-288993-000  
PT
Feedwater System
Check valve hinge pin seal weld.  
2047 foot elevation, RB C loop  
Drawing WOP-M-13AE04-008-A-1  
WO 08-305300-013
PT


        SYSTEM               WELD IDENTIFICATION         EXAMINATION
                                                            TYPE
Feedwater System     Check valve - flange to pipe weld       RT
- 20 -
                    joint. 2026 elevation of Area 5
                    WO 08-305300-048 and -049
Reactor Vessel       RPV meridonal welds,                   UT
Closure Head        ISI Number CH-101-104-B
Reactor Vessel       RPV meridonal weld,                     UT
Enclosure 2
Closure Head        ISI Number CH-101-104-C
SYSTEM  
High Pressure Safety HPSI pipe to elbow weld, ISI Number     UT
WELD IDENTIFICATION  
Injection            EM-03-S015-B
EXAMINATION
Residual Heat       Pipe to Pipe Weld,                     UT
TYPE  
Removal              ISI Number EJ-04-F019
Feedwater System  
Reactor Vessel       Reactor vessel washer and             VT - 1
Check valve - flange to pipe weld  
Closure Head        Bushings 19-24,
joint. 2026 elevation of Area 5  
                    Component CH-WASH 19-24
WO 08-305300-048 and -049  
                    Drawing M-189-50ISI-RBB01
RT
                    WO 08-311169-014
Reactor Vessel  
Safety Injection     Vent valve. Safety injection pump     VT - 1
Closure Head
                    Room A
RPV meridonal welds,  
                    Drawing WIP-M-13EM01-008-A-01
ISI Number CH-101-104-B  
                    WO 08-310289-068
UT
Reactor Vessel Head Required by 10FR50.55a, ASME           VT - 2
Reactor Vessel  
                    Code Case N-729-1. Also IEWA-2212
Closure Head
                    VT-2 under mirror insulation
RPV meridonal weld,  
                    WO 08-307175-001
ISI Number CH-101-104-C  
Piping Support       In containment                         VT- 3
UT
                    Component EJ-04-H002
High Pressure Safety  
                    WO 08-311169-001
Injection
Piping Support       In containment.                       VT- 3
HPSI pipe to elbow weld, ISI Number  
                    Component EM-03-C033
EM-03-S015-B  
                    WO 06-288978-001
UT
                            - 20 -                          Enclosure 2
Residual Heat  
Removal
Pipe to Pipe Weld,  
ISI Number EJ-04-F019  
UT
Reactor Vessel  
Closure Head
Reactor vessel washer and  
Bushings 19-24,  
Component CH-WASH 19-24  
Drawing M-189-50ISI-RBB01  
WO 08-311169-014  
VT - 1
Safety Injection  
Vent valve. Safety injection pump  
Room A  
Drawing WIP-M-13EM01-008-A-01  
WO 08-310289-068  
VT - 1
Reactor Vessel Head  
Required by 10FR50.55a, ASME  
Code Case N-729-1. Also IEWA-2212  
VT-2 under mirror insulation  
WO 08-307175-001  
VT - 2
Piping Support  
In containment
Component EJ-04-H002  
WO 08-311169-001  
VT- 3
Piping Support  
In containment.
Component EM-03-C033  
WO 06-288978-001  
VT- 3


        SYSTEM                     WELD IDENTIFICATION             EXAMINATION
                                                                            TYPE
Piping Support             In containment.                               VT- 3
- 21 -
                            Component BG-22-H007
                            WO 08-311169-011
During the review and observation of each examination, the inspectors verified that
activities were performed in accordance with ASME Boiler and Pressure Vessel Code
requirements and applicable procedures. During the observed nondestructive
Enclosure 2
examinations identified above, three relevant indications were identified (one dye
SYSTEM  
penetrant, one radiograph, and one boric acid leak on the control rod drive mechanism
WELD IDENTIFICATION  
canopy seal weld). Indications identified were dispositioned in accordance with ASME
EXAMINATION
Code and approved procedures. The two weld indications were removed and
TYPE  
re-examined. A control rod drive mechanism canopy seal weld clamp was installed.
Piping Support  
There were no examinations performed where relevant indications had been accepted
In containment.
by the licensee for continued service. The qualifications of all nondestructive
Component BG-22-H007  
examination technicians performing the inspections were verified to be current.
WO 08-311169-011  
The inspectors directly observed a portion of the following welding activities:
VT- 3
    SYSTEM               WELD IDENTIFICATION                   WELD TYPE
Reactor Coolant     Reactor coolant pump seal         Inlay, Gas Tungsten Arc
During the review and observation of each examination, the inspectors verified that  
Pump Seal            water supply line drain.           Welding, hand welded
activities were performed in accordance with ASME Boiler and Pressure Vessel Code  
Water                1974 foot elevation auxiliary
requirements and applicable procedures. During the observed nondestructive  
                      building, letdown heat
examinations identified above, three relevant indications were identified (one dye  
                      exchanger room.
penetrant, one radiograph, and one boric acid leak on the control rod drive mechanism  
                      WO 06-288993-000.
canopy seal weld). Indications identified were dispositioned in accordance with ASME  
High Pressure       Vent valve. 1974 foot elevation   Inlay, Gas Tungsten Arc
Code and approved procedures. The two weld indications were removed and  
Safety Injection    of auxiliary building, area 1.     Welding, hand welded
re-examined. A control rod drive mechanism canopy seal weld clamp was installed.
System              WO 08-310289-077
There were no examinations performed where relevant indications had been accepted  
Chemical and         Vent valve. Reactor water         Inlay, Gas Tungsten Arc
by the licensee for continued service. The qualifications of all nondestructive  
Volume Control      storage tank to centrifugal       Welding, hand welded
examination technicians performing the inspections were verified to be current.  
System              charging Pump A suction check
                      valve. 1974 foot elevation of
The inspectors directly observed a portion of the following welding activities:  
                      auxiliary building, area 1.
SYSTEM  
                      WO 08-310289-007
WELD IDENTIFICATION  
                                    - 21 -                                  Enclosure 2
WELD TYPE  
Reactor Coolant  
Pump Seal
Water
Reactor coolant pump seal  
water supply line drain.
1974 foot elevation auxiliary  
building, letdown heat  
exchanger room.  
WO 06-288993-000.  
Inlay, Gas Tungsten Arc
Welding, hand welded
High Pressure  
Safety Injection
System
Vent valve. 1974 foot elevation  
of auxiliary building, area 1.  
WO 08-310289-077
Inlay, Gas Tungsten Arc
Welding, hand welded
Chemical and  
Volume Control
System
Vent valve. Reactor water  
storage tank to centrifugal  
charging Pump A suction check  
valve. 1974 foot elevation of  
auxiliary building, area 1.  
WO 08-310289-007  
Inlay, Gas Tungsten Arc
Welding, hand welded


            SYSTEM             WELD IDENTIFICATION                     WELD TYPE
      Essential           Containment cooler B ESW             Inlay, Gas Tungsten Arc
      Service Water        supply isolation valve (install       Welding, hand welded
- 22 -
      System              flanges on pipe for butterfly
                            valve). 2047 foot elevation in
                            containment, near Cooler B
                            duct. WO 07-299593-012.
      Chemical and         Vent valve. Safety Injection         Inlay, Gas Tungsten Arc
Enclosure 2
      Volume Control      Pump Room B                           Welding, hand welded
SYSTEM  
      System              Valves BG-V0842 and V0843.
WELD IDENTIFICATION  
                            1974 foot elevation of auxiliary
WELD TYPE  
                            building, area 1.
Essential  
                            WO 08-310289-043.
Service Water
      The inspectors verified, by review, that the welding procedure specifications and the
System
      welders had been properly qualified in accordance with ASME Code, Section IX,
Containment cooler B ESW  
      requirements. The inspectors also verified through record review that essential variables
supply isolation valve (install  
      for the welding process were identified, recorded in the procedure qualification record,
flanges on pipe for butterfly  
      and formed the bases for qualification of the welding procedure specifications. Specific
valve). 2047 foot elevation in  
      documents reviewed during this inspection are listed in the attachment.
containment, near Cooler B  
      These actions constitute completion of the requirements for Section 02.01 of Inspection
duct. WO 07-299593-012.  
      Procedure IP 71111.08.
Inlay, Gas Tungsten Arc
  b. Findings:
Welding, hand welded
      A finding involving control of transient ignition sources is described in Section 1RO5.2 of
Chemical and  
      this report.
Volume Control
.2   Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)
System
  a. Inspection Scope
Vent valve. Safety Injection  
      The inspectors witnessed the licensees performance of the required visual inspection
Pump Room B  
      (VT-2) of the reactor head and pressure-retaining components above the reactor
Valves BG-V0842 and V0843.
      pressure vessel head in accordance with requirement of ASME Code Case N-729-1 as
1974 foot elevation of auxiliary  
      mandated by 10 CFR 50.55a effective October 10, 2008. Implementation required
building, area 1.  
      ASME Code IWA-2212 VT-2 under the mirror insulation on top of the reactor head
WO 08-310289-043.  
      through multiple access points. The inspectors reviewed the results of this inspection for
Inlay, Gas Tungsten Arc
      evidence of leaks or boron deposits at reactor pressure boundaries and related
Welding, hand welded
      insulation above the head. Specific documents reviewed during this inspection are listed
      in the attachment.
The inspectors verified, by review, that the welding procedure specifications and the  
                                          - 22 -                                  Enclosure 2
welders had been properly qualified in accordance with ASME Code, Section IX,  
requirements. The inspectors also verified through record review that essential variables  
for the welding process were identified, recorded in the procedure qualification record,  
and formed the bases for qualification of the welding procedure specifications. Specific  
documents reviewed during this inspection are listed in the attachment.  
These actions constitute completion of the requirements for Section 02.01 of Inspection  
Procedure IP 71111.08.  
b.  
Findings:  
A finding involving control of transient ignition sources is described in Section 1RO5.2 of  
this report.  
.2  
Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)  
a.  
Inspection Scope  
The inspectors witnessed the licensees performance of the required visual inspection  
(VT-2) of the reactor head and pressure-retaining components above the reactor  
pressure vessel head in accordance with requirement of ASME Code Case N-729-1 as  
mandated by 10 CFR 50.55a effective October 10, 2008. Implementation required  
ASME Code IWA-2212 VT-2 under the mirror insulation on top of the reactor head  
through multiple access points. The inspectors reviewed the results of this inspection for  
evidence of leaks or boron deposits at reactor pressure boundaries and related  
insulation above the head. Specific documents reviewed during this inspection are listed  
in the attachment.  


      These actions constitute completion of the requirements for Section 02.02 of Inspection
      Procedure PI 71111.08.
  b.  Findings
- 23 -
      No findings of significance were identified.
.3   Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)
  a. Inspection Scope:
      The inspectors evaluated the implementation of the licensees boric acid corrosion
      control program for monitoring degradation of those systems that could be adversely
Enclosure 2
      affected by boric acid corrosion. The inspection procedure required review of plant
      areas that had recently received a boric acid walkdown by the licensee, through either
These actions constitute completion of the requirements for Section 02.02 of Inspection  
      direct observation or record review. The inspectors reviewed the records associated with
Procedure PI 71111.08.  
      the licensees most recent boric acid corrosion control walkdown, as specified in
b.  
      Procedure STN PE-040D, "RCS Pressure Boundary Integrity Walkdown, Revision 3.
Findings
      The inspectors directly observed some of those plant areas recently walked down by the
   
      licensee. Additionally, the inspectors independently walked down piping and
No findings of significance were identified.  
      components containing boric acid inside containment and the auxiliary building. The
      inspection procedure also required verification that visual inspections emphasize
.3  
      locations where boric acid leaks can cause degradation of safety-significant components.
Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)  
      The inspectors verified through record review that the boric acid corrosion control
a.  
      inspection efforts were directed towards locations where boric acid leaks can cause
Inspection Scope:  
      degradation of safety-related components.
The inspectors evaluated the implementation of the licensees boric acid corrosion  
      The inspection procedure required review of one to three engineering evaluations
control program for monitoring degradation of those systems that could be adversely  
      performed for boric acid found on reactor coolant system piping and components. For
affected by boric acid corrosion. The inspection procedure required review of plant  
      those sources of boron leakage identified, the engineering evaluations gave assurance
areas that had recently received a boric acid walkdown by the licensee, through either  
      that the ASME Code wall thickness limits were properly maintained. The inspection
direct observation or record review. The inspectors reviewed the records associated with  
      procedure also required review of one to three corrective actions performed for evidence
the licensees most recent boric acid corrosion control walkdown, as specified in  
      of boric acid leaks identified. The inspectors confirmed that the work orders and
Procedure STN PE-040D, "RCS Pressure Boundary Integrity Walkdown, Revision 3.
      evaluations generated in response to boron leakage identification were consistent with
The inspectors directly observed some of those plant areas recently walked down by the  
      requirements of the ASME Code and 10 CFR Part 50, Appendix B, Criterion XVI.
licensee. Additionally, the inspectors independently walked down piping and  
      Specific documents reviewed during this inspection are listed in the attachment.
components containing boric acid inside containment and the auxiliary building. The  
      These actions constitute completion of the requirements for Section 02.03 of Inspection
inspection procedure also required verification that visual inspections emphasize  
      Procedure IP 71111.08
locations where boric acid leaks can cause degradation of safety-significant components.
  b. Findings
The inspectors verified through record review that the boric acid corrosion control  
      Introduction. The inspectors identified a noncited violation of 10 CFR Part 50,
inspection efforts were directed towards locations where boric acid leaks can cause  
      Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees
degradation of safety-related components.  
      failure to identify sources of boron leakage and document them in a corrective action
      document. Specifically, during a boric acid walkdown, the inspectors identified
The inspection procedure required review of one to three engineering evaluations  
                                          - 23 -                                Enclosure 2
performed for boric acid found on reactor coolant system piping and components. For  
those sources of boron leakage identified, the engineering evaluations gave assurance  
that the ASME Code wall thickness limits were properly maintained. The inspection  
procedure also required review of one to three corrective actions performed for evidence  
of boric acid leaks identified. The inspectors confirmed that the work orders and  
evaluations generated in response to boron leakage identification were consistent with  
requirements of the ASME Code and 10 CFR Part 50, Appendix B, Criterion XVI.
Specific documents reviewed during this inspection are listed in the attachment.  
These actions constitute completion of the requirements for Section 02.03 of Inspection  
Procedure IP 71111.08  
b.  
Findings  
Introduction. The inspectors identified a noncited violation of 10 CFR Part 50,  
Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees  
failure to identify sources of boron leakage and document them in a corrective action  
document. Specifically, during a boric acid walkdown, the inspectors identified  


11 sources of boron leakage which had not been previously identified and documented
by the licensee.
Description. On October 23, 2009, the inspectors performed a boric acid walkdown of
- 24 -
areas inside containment and the auxiliary building. The inspectors identified 11 sources
of leakage which had not been previously identified and documented in a corrective
action document by the licensee during the licensees boric acid walkdowns completed
on October 11, 2009. With the exception of one leak, the leaks were not active and only
had small amounts of boric acid crystals present.
Enclosure 2
The inspectors noted that those boron leakage sources which were identified during the
11 sources of boron leakage which had not been previously identified and documented  
walkdown inside containment were described by the licensee in the completed
by the licensee.  
walkdown procedure as having no boron indication. The licensee stated that their boric
acid inspections were focused on larger amounts of boron leakage and may have been
insensitive to smaller amounts of leakage. This is contrary to station
Description. On October 23, 2009, the inspectors performed a boric acid walkdown of  
Procedure AP 16F-001, "Boric Acid Corrosion Control Program," Revision 5, step 6.4.1,
areas inside containment and the auxiliary building. The inspectors identified 11 sources  
which states that: Sources of boron seepage/leakage shall be identified/verified and
of leakage which had not been previously identified and documented in a corrective  
documented in the applicable corrective action document. The licensee entered the
action document by the licensee during the licensees boric acid walkdowns completed  
missed leakage sources into their corrective action program and initiated a condition
on October 11, 2009. With the exception of one leak, the leaks were not active and only  
report to follow up on the extent of condition of missed boron leakage sources.
had small amounts of boric acid crystals present.  
Analysis. The inspectors determined that the failure to identify sources of boron leakage
was contrary to station procedures and was a performance deficiency. Specifically,
11 examples of boron leakage were not identified and documented in a corrective action
The inspectors noted that those boron leakage sources which were identified during the  
document.
walkdown inside containment were described by the licensee in the completed  
The finding was determined to be more than minor in accordance with Inspection
walkdown procedure as having no boron indication. The licensee stated that their boric  
Manual Chapter 0612, Appendix B, Issue Screening, because it was associated with
acid inspections were focused on larger amounts of boron leakage and may have been  
the human performance attribute of the Initiating Events Cornerstone and affected the
insensitive to smaller amounts of leakage. This is contrary to station  
cornerstone objective of limiting the likelihood of those events that upset plant stability
Procedure AP 16F-001, "Boric Acid Corrosion Control Program," Revision 5, step 6.4.1,  
and challenge critical safety functions during shutdown as well as power operations.
which states that: Sources of boron seepage/leakage shall be identified/verified and  
Specifically, boric acid leakage has historically been found to degrade carbon steel
documented in the applicable corrective action document. The licensee entered the  
components which could affect the reactor coolant system pressure boundary or impact
missed leakage sources into their corrective action program and initiated a condition  
the reliability of emergency core cooling systems. The inspectors used Inspection
report to follow up on the extent of condition of missed boron leakage sources.  
Manual Chapter 0609, Significance Determination Process, Attachment 4, Phase 1 -
Initial Screening and Characterization of Findings, and determined the finding was of
very low safety significance (Green) because the issue would not result in exceeding the
Analysis. The inspectors determined that the failure to identify sources of boron leakage  
technical specification limit for identified reactor coolant system leakage or effect other
was contrary to station procedures and was a performance deficiency. Specifically,  
mitigating systems resulting in a total loss of their safety function. The inspectors also
11 examples of boron leakage were not identified and documented in a corrective action  
determined that the finding had a crosscutting aspect in the area of problem
document.  
identification and resolution, operating experience, where the licensee did not
institutionalizes operating experience through changes to station processes, procedures,
equipment, and training programs [P.2.(b)].
The finding was determined to be more than minor in accordance with Inspection  
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
Manual Chapter 0612, Appendix B, Issue Screening, because it was associated with  
and Drawings, states, in part, that Activities affecting quality shall be prescribed by
the human performance attribute of the Initiating Events Cornerstone and affected the  
documented instructions, procedures, or drawings, of a type appropriate to the
cornerstone objective of limiting the likelihood of those events that upset plant stability  
                                      - 24 -                                    Enclosure 2
and challenge critical safety functions during shutdown as well as power operations.
Specifically, boric acid leakage has historically been found to degrade carbon steel  
components which could affect the reactor coolant system pressure boundary or impact  
the reliability of emergency core cooling systems. The inspectors used Inspection  
Manual Chapter 0609, Significance Determination Process, Attachment 4, Phase 1 -  
Initial Screening and Characterization of Findings, and determined the finding was of  
very low safety significance (Green) because the issue would not result in exceeding the  
technical specification limit for identified reactor coolant system leakage or effect other  
mitigating systems resulting in a total loss of their safety function. The inspectors also  
determined that the finding had a crosscutting aspect in the area of problem  
identification and resolution, operating experience, where the licensee did not  
institutionalizes operating experience through changes to station processes, procedures,  
equipment, and training programs [P.2.(b)].
 
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
and Drawings, states, in part, that Activities affecting quality shall be prescribed by  
documented instructions, procedures, or drawings, of a type appropriate to the  


      circumstances and shall be accomplished in accordance with these instructions,
      procedures, or drawings. Licensee Procedure AP 16F-001,"Boric Acid Corrosion
      Control Program," Revision 5, which prescribes activities affecting quality, states, in part,
- 25 -
      that sources of boron seepage/leakage shall be identified/verified and documented in
      the applicable corrective action document. Contrary to the above, prior to October 23,
      2009, the licensee failed to accomplish the requirements of Procedure AP 16F-001.
      Specifically, the licensee failed to identify 11 sources of boron leakage in the containment
      structure and the auxiliary building and document them in a corrective action document.
Enclosure 2
      Because this issue was determined to be of very low safety significance (Green) and
circumstances and shall be accomplished in accordance with these instructions,  
      was entered into the licensees corrective action program as Condition
procedures, or drawings. Licensee Procedure AP 16F-001,"Boric Acid Corrosion  
      Report AR-00021274, this violation is being treated as a noncited violation in accordance
Control Program," Revision 5, which prescribes activities affecting quality, states, in part,  
      with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2009005-03,
that sources of boron seepage/leakage shall be identified/verified and documented in  
      Failure to Identify Sources of Boron Leakage.
the applicable corrective action document. Contrary to the above, prior to October 23,  
.4   Steam Generator Tube Inspection Activities (71111.08-02.04)
2009, the licensee failed to accomplish the requirements of Procedure AP 16F-001.
  a. Inspection Scope:
Specifically, the licensee failed to identify 11 sources of boron leakage in the containment  
      The inspection procedure specified performance of an assessment of in situ screening
structure and the auxiliary building and document them in a corrective action document.
      criteria to assure consistency between assumed nondestructive examination flaw sizing
Because this issue was determined to be of very low safety significance (Green) and  
      accuracy and data from the EPRI examination technique specification sheets. It further
was entered into the licensees corrective action program as Condition  
      specified assessment of appropriateness of tubes selected for in situ pressure testing,
Report AR-00021274, this violation is being treated as a noncited violation in accordance  
      observation of in situ pressure testing, and review of in situ pressure test results.
with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2009005-03,  
      At the time of this inspection, no conditions had been identified that warranted in situ
Failure to Identify Sources of Boron Leakage.  
      pressure testing. The inspectors reviewed the Licensees Report SG-CDME-08-15,
.4  
      Wolf Creek Refueling 16 Condition Monitoring Assessment and Operational
Steam Generator Tube Inspection Activities (71111.08-02.04)  
      Assessment, Revision 1, dated April 2008, and compared the in situ test screening
a.  
      parameters to the guidelines contained in the EPRI document In Situ Pressure Test
Inspection Scope:  
      Guidelines, Revision 2. This review determined that the remaining screening
      parameters were consistent with the EPRI guidelines.
The inspection procedure specified performance of an assessment of in situ screening  
      In addition, the inspectors reviewed both the licensee site-validated and qualified
criteria to assure consistency between assumed nondestructive examination flaw sizing  
      acquisition and analysis technique sheets used during this refueling outage and the
accuracy and data from the EPRI examination technique specification sheets. It further  
      qualifying EPRI examination technique specification sheets to verify that the essential
specified assessment of appropriateness of tubes selected for in situ pressure testing,  
      variables regarding flaw sizing accuracy, tubing, equipment, technique, and analysis had
observation of in situ pressure testing, and review of in situ pressure test results.
      been identified and qualified through demonstration. The inspector-reviewed acquisition
      technique and analysis technique sheets are identified in the attachment.
At the time of this inspection, no conditions had been identified that warranted in situ  
      The inspection procedure specified comparing the estimated size and number of tube
pressure testing. The inspectors reviewed the Licensees Report SG-CDME-08-15,  
      flaws detected during the current outage against the previous outage operational
Wolf Creek Refueling 16 Condition Monitoring Assessment and Operational  
      assessment predictions to assess the licensees prediction capability. The inspectors
Assessment, Revision 1, dated April 2008, and compared the in situ test screening  
      compared the previous outage operational assessment predictions contained in
parameters to the guidelines contained in the EPRI document In Situ Pressure Test  
      Report SG-CDME-08-15, Revision 1, with the flaws identified thus far during the current
Guidelines, Revision 2. This review determined that the remaining screening  
      steam generator tube inspection effort. Compared to the projected damage
parameters were consistent with the EPRI guidelines.  
      mechanisms identified by the licensee, the number of identified indications fell within the
      range of prediction and was quite consistent with predictions.
In addition, the inspectors reviewed both the licensee site-validated and qualified  
                                            - 25 -                                  Enclosure 2
acquisition and analysis technique sheets used during this refueling outage and the  
qualifying EPRI examination technique specification sheets to verify that the essential  
variables regarding flaw sizing accuracy, tubing, equipment, technique, and analysis had  
been identified and qualified through demonstration. The inspector-reviewed acquisition  
technique and analysis technique sheets are identified in the attachment.
The inspection procedure specified comparing the estimated size and number of tube  
flaws detected during the current outage against the previous outage operational  
assessment predictions to assess the licensees prediction capability. The inspectors  
compared the previous outage operational assessment predictions contained in  
Report SG-CDME-08-15, Revision 1, with the flaws identified thus far during the current  
steam generator tube inspection effort. Compared to the projected damage  
mechanisms identified by the licensee, the number of identified indications fell within the  
range of prediction and was quite consistent with predictions.  


  The inspection procedure specified confirmation that the steam generator tube test
  scope and expansion criteria meet technical specification requirements, EPRI
  guidelines, and commitments made to the NRC. The inspectors evaluated the
- 26 -
  recommended steam generator tube eddy current test scope established by technical
  specification requirements. The inspectors compared the recommended test scope to
  the actual test scope and found that the licensee had accounted for all known flaws and
  had established a test scope that met or exceeded minimum technical specification
  requirements, EPRI guidelines, and commitments made to the NRC. The scope of the
Enclosure 2
  licensees Eddy current examinations of tubes in both steam generators included:
* 100 percent, bobbin examination of tubes in steam generators A and D, full length
The inspection procedure specified confirmation that the steam generator tube test  
  except for rows 1 and 2, which were inspected with the bobbin from tube end to tube
scope and expansion criteria meet technical specification requirements, EPRI  
  support plate 7 from both hot and cold legs
guidelines, and commitments made to the NRC. The inspectors evaluated the  
* 50 percent, Rows 1 and 2 U-bends, mid-range +Point examination in steam
recommended steam generator tube eddy current test scope established by technical  
  generators A and D
specification requirements. The inspectors compared the recommended test scope to  
* Mid-range +Point examination of 100 percent of the cold leg peripheral tubes in steam
the actual test scope and found that the licensee had accounted for all known flaws and  
  generators A and D
had established a test scope that met or exceeded minimum technical specification  
* Dings (free span) > 5 volts: inspect 50 percent of all previously identified and new dings
requirements, EPRI guidelines, and commitments made to the NRC. The scope of the  
  >5 volts in the hot leg (including the U-bends) with the mid-range +Point probe in steam
licensees Eddy current examinations of tubes in both steam generators included:
  generators A and D
*  
* Dents (structures) > 2 volts: inspect 50 percent of all previously identified and new dents
100 percent, bobbin examination of tubes in steam generators A and D, full length  
  >2 volts in the hot leg (including the U-bends) with the mid-range +Point probe in steam
except for rows 1 and 2, which were inspected with the bobbin from tube end to tube  
  generators A and D
support plate 7 from both hot and cold legs
* +Point examination of all "I-code" indications that were not resolved after history review
*  
* +Point inspection of new wear indications and prior wear indications that have changed
50 percent, Rows 1 and 2 U-bends, mid-range +Point examination in steam  
  by 10 percent through-wall defect or greater in steam generators A and D
generators A and D
* Visual inspection of mechanical and weld plugs
*  
* +Point examination of a five percent sample of bobbin indications that have not changed
Mid-range +Point examination of 100 percent of the cold leg peripheral tubes in steam  
  since the prior inspection (H and S codes)
generators A and D
* +Point inspection to bound (all surrounding tubes, at least one pitch removed) the tubes
*  
  exhibiting possible loose parts signals during the inspection
Dings (free span) > 5 volts: inspect 50 percent of all previously identified and new dings  
* +Point inspection of a sample of tubes to support the scale profiling effort
>5 volts in the hot leg (including the U-bends) with the mid-range +Point probe in steam  
  The results, as known to the inspectors at the conclusion of this inspection, are as
generators A and D
  follows:
*  
  For steam generator A, 6 tubes with wear indication of 40 percent through-wall defect or
Dents (structures) > 2 volts: inspect 50 percent of all previously identified and new dents  
  greater at one or more anti-vibration bar intersections were plugged. Additionally, one
>2 volts in the hot leg (including the U-bends) with the mid-range +Point probe in steam  
  tube was conservatively plugged for a geometric anomaly. This tube did not exhibit any
generators A and D
  cracking characteristic after analysis of the +Point and Ghent probe data.
*  
                                      - 26 -                                  Enclosure 2
+Point examination of all "I-code" indications that were not resolved after history review
*  
+Point inspection of new wear indications and prior wear indications that have changed  
by 10 percent through-wall defect or greater in steam generators A and D
*  
Visual inspection of mechanical and weld plugs  
*  
+Point examination of a five percent sample of bobbin indications that have not changed  
since the prior inspection (H and S codes)  
*  
+Point inspection to bound (all surrounding tubes, at least one pitch removed) the tubes  
exhibiting possible loose parts signals during the inspection  
*  
+Point inspection of a sample of tubes to support the scale profiling effort  
The results, as known to the inspectors at the conclusion of this inspection, are as  
follows:
For steam generator A, 6 tubes with wear indication of 40 percent through-wall defect or  
greater at one or more anti-vibration bar intersections were plugged. Additionally, one  
tube was conservatively plugged for a geometric anomaly. This tube did not exhibit any  
cracking characteristic after analysis of the +Point and Ghent probe data.  


  For steam generator D, 10 tubes with wear indication of 40 percent through-wall defect
   
or greater at one or more anti-vibration bar intersections were plugged. Additionally, one
tube was conservatively plugged for a geometric anomaly. This tube did not exhibit any
- 27 -
cracking characteristic after analysis of the +Point and Ghent probe data.
The inspection procedure specified that, if new degradation mechanisms were identified,
the licensee would verify the analysis fully enveloped the problem of the extended
conditions including operating concerns and that appropriate corrective actions were
taken before plant startup. No new degradation mechanisms were identified by the
Enclosure 2
eddy current examination results.
  The inspection procedure required confirmation that the licensee inspected all areas of
For steam generator D, 10 tubes with wear indication of 40 percent through-wall defect  
potential degradation, especially areas that were known to represent potential eddy
or greater at one or more anti-vibration bar intersections were plugged. Additionally, one  
current test challenges (e.g., top of tube sheet, tube support plates, and U-bends). The
tube was conservatively plugged for a geometric anomaly. This tube did not exhibit any  
inspectors confirmed that all known areas of potential degradation were included in the
cracking characteristic after analysis of the +Point and Ghent probe data.  
scope of inspection and were being inspected.
The inspection procedure specified that, if new degradation mechanisms were identified,  
  The inspection procedure further required verification that repair processes being used
the licensee would verify the analysis fully enveloped the problem of the extended  
were approved in the technical specifications. At the completion of the inspection, the
conditions including operating concerns and that appropriate corrective actions were  
inspectors were informed that 18 tubes were to be plugged. The inspectors verified that
taken before plant startup. No new degradation mechanisms were identified by the  
the mechanical expansion plugging process used was an NRC-approved repair process.
eddy current examination results.
The inspection procedure also required confirmation of adherence to the technical
  The inspection procedure required confirmation that the licensee inspected all areas of  
specification plugging limit, unless alternate repair criteria had been approved. The
potential degradation, especially areas that were known to represent potential eddy  
inspection procedure further requires determination whether depth sizing repair criteria
current test challenges (e.g., top of tube sheet, tube support plates, and U-bends). The  
were being applied for indications other than wear or axial primary water stress corrosion
inspectors confirmed that all known areas of potential degradation were included in the  
cracking in dented tube support plate intersections. The inspectors determined that the
scope of inspection and were being inspected.  
technical specification plugging limits were being adhered to (i.e., 40 percent maximum
  The inspection procedure further required verification that repair processes being used  
through-wall indication).
were approved in the technical specifications. At the completion of the inspection, the  
If steam generator leakage greater than three gallons per day was identified during
inspectors were informed that 18 tubes were to be plugged. The inspectors verified that  
operations or during post shutdown visual inspections of the tube sheet face, the
the mechanical expansion plugging process used was an NRC-approved repair process.
inspection procedure required verification that the licensee had identified a reasonable
cause based on inspection results and that corrective actions were taken or planned to
The inspection procedure also required confirmation of adherence to the technical  
address the cause for the leakage. The inspectors did not conduct any assessment
specification plugging limit, unless alternate repair criteria had been approved. The  
because this condition did not exist.
inspection procedure further requires determination whether depth sizing repair criteria  
The inspection procedure required confirmation that the eddy current test probes and
were being applied for indications other than wear or axial primary water stress corrosion  
equipment were qualified for the expected types of tube degradation and an assessment
cracking in dented tube support plate intersections. The inspectors determined that the  
of the site-specific qualification of one or more techniques. The inspectors observed
technical specification plugging limits were being adhered to (i.e., 40 percent maximum  
portions of eddy current tests performed on the tubes in steam generators A and D.
through-wall indication).
During these examinations, the inspectors verified that: (1) the probes appropriate for
identifying the expected types of indications were being used, (2) probe position location
verification was performed, (3) calibration requirements were adhered to, and (4) probe
If steam generator leakage greater than three gallons per day was identified during  
travel speed was in accordance with procedural requirements. The inspectors
operations or during post shutdown visual inspections of the tube sheet face, the  
performed a review of site-specific qualifications of the techniques being used. These
inspection procedure required verification that the licensee had identified a reasonable  
are identified in the attachment.
cause based on inspection results and that corrective actions were taken or planned to  
                                      - 27 -                                Enclosure 2
address the cause for the leakage. The inspectors did not conduct any assessment  
because this condition did not exist.
The inspection procedure required confirmation that the eddy current test probes and  
equipment were qualified for the expected types of tube degradation and an assessment  
of the site-specific qualification of one or more techniques. The inspectors observed  
portions of eddy current tests performed on the tubes in steam generators A and D.
During these examinations, the inspectors verified that: (1) the probes appropriate for  
identifying the expected types of indications were being used, (2) probe position location  
verification was performed, (3) calibration requirements were adhered to, and (4) probe  
travel speed was in accordance with procedural requirements. The inspectors  
performed a review of site-specific qualifications of the techniques being used. These  
are identified in the attachment.  


      The inspection procedure specified that if loose parts or foreign materials were identified
      on the secondary side, the inspectors should review the licensee's evaluation of the
      materials and/or complete appropriate repairs of affected steam generator tubes.
- 28 -
      Additionally, the licensee should either remove accessible foreign objects or perform an
      evaluation of the potential effects of inaccessible object migration and tube fretting
      damage. During this inspection, 18 small foreign objects were found in steam
      generator A; of these, 7 items were retrieved. There were 34 small foreign objects found
      in steam generator D; of these, 18 items were retrieved. These objects, small wires and
Enclosure 2
      sludge rocks, were prioritized and retrieved based on their potential to damage the
      steam generator tubes in accordance with Refuel Outage 17 Degradation Assessment
The inspection procedure specified that if loose parts or foreign materials were identified  
      and EPRI 1019039, Steam Generator Management Program: Foreign Object
on the secondary side, the inspectors should review the licensee's evaluation of the  
      Prioritization Strategy for Square Pitch Steam Generators. Those items not removed
materials and/or complete appropriate repairs of affected steam generator tubes.
      from the steam generators were evaluated and determined to have no ability to damage
Additionally, the licensee should either remove accessible foreign objects or perform an  
      the steam generator tubes during operation. Condition Report AR-00021178 documents
evaluation of the potential effects of inaccessible object migration and tube fretting  
      the foreign objects in the licensee's corrective action program. The required chemical
damage. During this inspection, 18 small foreign objects were found in steam  
      and mechanical effects of these remaining pieces were analyzed with the conclusion of
generator A; of these, 7 items were retrieved. There were 34 small foreign objects found  
      negligible effects on the respective steam generators. Work Orders 09-321481-000 and
in steam generator D; of these, 18 items were retrieved. These objects, small wires and  
      09-321386-000 evaluated the acceptability of the steam generators with these minor
sludge rocks, were prioritized and retrieved based on their potential to damage the  
      foreign objects remaining.
steam generator tubes in accordance with Refuel Outage 17 Degradation Assessment  
      Finally, the inspection procedure specified review of one-to-five samples of eddy current
and EPRI 1019039, Steam Generator Management Program: Foreign Object  
      test data if questions arose regarding the adequacy of eddy current test data analyses.
Prioritization Strategy for Square Pitch Steam Generators. Those items not removed  
      The inspectors did not identify any results where eddy current test data analyses
from the steam generators were evaluated and determined to have no ability to damage  
      adequacy was questionable.
the steam generator tubes during operation. Condition Report AR-00021178 documents  
      These actions constitute completion of the requirements for Section 02.04 of Inspection
the foreign objects in the licensee's corrective action program. The required chemical  
      Procedure IP 71111.08.
and mechanical effects of these remaining pieces were analyzed with the conclusion of  
  b. Findings
negligible effects on the respective steam generators. Work Orders 09-321481-000 and  
      No findings of significance were identified.
09-321386-000 evaluated the acceptability of the steam generators with these minor  
.5   Identification and Resolution of Problems (71111.08-02.05)
foreign objects remaining.
  a. Inspection Scope
      The inspection procedure required review of a sample of problems associated with
      inservice inspections documented by the licensee in the corrective action program for
      appropriateness of the corrective actions.
Finally, the inspection procedure specified review of one-to-five samples of eddy current  
      The inspectors reviewed nine condition reports which dealt with inservice inspection
test data if questions arose regarding the adequacy of eddy current test data analyses.
      activities and found the corrective actions were appropriate. The specific condition
The inspectors did not identify any results where eddy current test data analyses  
      reports reviewed are listed in the documents reviewed section. From this review, the
adequacy was questionable.
      inspectors concluded that the licensee has an appropriate threshold for entering issues
      into the corrective action program and has procedures that direct a root cause evaluation
      when necessary. The licensee also has an effective program for applying industry
These actions constitute completion of the requirements for Section 02.04 of Inspection  
                                          - 28 -                                  Enclosure 2
Procedure IP 71111.08.  
b.  
Findings  
No findings of significance were identified.  
.5  
Identification and Resolution of Problems (71111.08-02.05)  
a.  
Inspection Scope  
The inspection procedure required review of a sample of problems associated with  
inservice inspections documented by the licensee in the corrective action program for  
appropriateness of the corrective actions.  
The inspectors reviewed nine condition reports which dealt with inservice inspection  
activities and found the corrective actions were appropriate. The specific condition  
reports reviewed are listed in the documents reviewed section. From this review, the  
inspectors concluded that the licensee has an appropriate threshold for entering issues  
into the corrective action program and has procedures that direct a root cause evaluation  
when necessary. The licensee also has an effective program for applying industry  


    operating experience. Specific documents reviewed during this inspection are listed in
    the attachment.
    These actions constitute completion of the requirements for Section 02.05 of Inspection
- 29 -
    Procedure IP 71111.08.
  b. Findings:
    No findings of significance were identified.
1R11 Licensed Operator Requalification Program (71111.11)
  a. Inspection Scope
Enclosure 2
    There were no opportunities to inspect operator requalification in the fourth quarter.
operating experience. Specific documents reviewed during this inspection are listed in  
    There were zero activities completed for quarterly licensed-operator requalification as
the attachment.  
    defined in Inspection Procedure IP 71111.11.
  b. Findings
These actions constitute completion of the requirements for Section 02.05 of Inspection  
    No findings of significance were identified.
Procedure IP 71111.08.  
1R12 Maintenance Effectiveness (71111.12)
  a. Inspection Scope
b.  
    The inspectors evaluated degraded performance issues involving the following risk
Findings:  
    significant systems:
No findings of significance were identified.  
    *       October 27, 2009, 125Vdc nonsafety-related PK system
    *       December 17, 2009, Component cooling water system
1R11 Licensed Operator Requalification Program (71111.11)  
    *       December 18, 2009, Source range neutron monitors
a.  
    *       October 6, 2009, Residual heat removal system
Inspection Scope  
    *       December 21, 2009, Offsite power supplies
There were no opportunities to inspect operator requalification in the fourth quarter.  
    *       December 22, 2009, Intermediate range neutron monitors
There were zero activities completed for quarterly licensed-operator requalification as  
    The inspectors reviewed events such as where ineffective equipment maintenance has
defined in Inspection Procedure IP 71111.11.  
    resulted in valid or invalid automatic actuations of engineered safeguards systems and
b.  
    independently verified the licensee's actions to address system performance or condition
Findings  
    problems in terms of the following:
No findings of significance were identified.  
    *       Implementing appropriate work practices
    *       Identifying and addressing common cause failures
1R12 Maintenance Effectiveness (71111.12)
    *       Scoping of systems in accordance with 10 CFR 50.65(b)
a.  
                                        - 29 -                                  Enclosure 2
Inspection Scope  
The inspectors evaluated degraded performance issues involving the following risk  
significant systems:  
*  
October 27, 2009, 125Vdc nonsafety-related PK system
*  
December 17, 2009, Component cooling water system  
*  
December 18, 2009, Source range neutron monitors  
*  
October 6, 2009, Residual heat removal system  
*  
December 21, 2009, Offsite power supplies  
*  
December 22, 2009, Intermediate range neutron monitors  
The inspectors reviewed events such as where ineffective equipment maintenance has  
resulted in valid or invalid automatic actuations of engineered safeguards systems and  
independently verified the licensee's actions to address system performance or condition  
problems in terms of the following:  
*  
Implementing appropriate work practices  
*  
Identifying and addressing common cause failures  
*  
Scoping of systems in accordance with 10 CFR 50.65(b)  


    *       Characterizing system reliability issues for performance
    *       Charging unavailability for performance
    *       Trending key parameters for condition monitoring
- 30 -
    *       Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)
    *       Verifying appropriate performance criteria for structures, systems, and
              components classified as having an adequate demonstration of performance
              through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as
              requiring the establishment of appropriate and adequate goals and corrective
Enclosure 2
              actions for systems classified as not having adequate performance, as described
*  
              in 10 CFR 50.65(a)(1)
Characterizing system reliability issues for performance  
    The inspectors assessed performance issues with respect to the reliability, availability,
*  
    and condition monitoring of the system. In addition, the inspectors verified maintenance
Charging unavailability for performance  
    effectiveness issues were entered into the corrective action program with the appropriate
*  
    significance characterization. Specific documents reviewed during this inspection are
Trending key parameters for condition monitoring  
    listed in the attachment.
*  
    These activities constitute completion of six quarterly maintenance effectiveness
Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)  
    samples as defined in Inspection Procedure IP 71111.12-05.
*  
  b. Findings
Verifying appropriate performance criteria for structures, systems, and  
    No findings of significance were identified.
components classified as having an adequate demonstration of performance  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as  
  a. Inspection Scope
requiring the establishment of appropriate and adequate goals and corrective  
    The inspectors reviewed licensee personnel's evaluation and management of plant risk
actions for systems classified as not having adequate performance, as described  
    for the maintenance and emergent work activities affecting risk-significant and safety-
in 10 CFR 50.65(a)(1)  
    related equipment listed below to verify that the appropriate risk assessments were
The inspectors assessed performance issues with respect to the reliability, availability,  
    performed prior to removing equipment for work:
and condition monitoring of the system. In addition, the inspectors verified maintenance  
    *       November 20, 2009, Emergent work on control room door ventilation boundary
effectiveness issues were entered into the corrective action program with the appropriate  
    *       October 15, 2009, Corrosion on containment cooler A
significance characterization. Specific documents reviewed during this inspection are  
    *       October 13, 2009, Emergent work on annunciator power supply failures
listed in the attachment.  
    *       October 10 to November 17, 2009, Shutdown risk assessments
These activities constitute completion of six quarterly maintenance effectiveness  
    *       November 18, 2009, Technical Specification 3.0.4.b risk assessment for Mode 4
samples as defined in Inspection Procedure IP 71111.12-05.  
              to Mode 3
b.  
    *       November 23, 2009, Emergent work for oil loss from centrifugal charging pump A
Findings  
                                          - 30 -                                  Enclosure 2
No findings of significance were identified.  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
a.  
Inspection Scope  
The inspectors reviewed licensee personnel's evaluation and management of plant risk  
for the maintenance and emergent work activities affecting risk-significant and safety-
related equipment listed below to verify that the appropriate risk assessments were  
performed prior to removing equipment for work:  
*  
November 20, 2009, Emergent work on control room door ventilation boundary  
*  
October 15, 2009, Corrosion on containment cooler A  
*  
October 13, 2009, Emergent work on annunciator power supply failures  
*  
October 10 to November 17, 2009, Shutdown risk assessments  
*  
November 18, 2009, Technical Specification 3.0.4.b risk assessment for Mode 4  
to Mode 3  
*  
November 23, 2009, Emergent work for oil loss from centrifugal charging pump A  


      The inspectors selected these activities based on potential risk significance relative to
      the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified
      that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)
- 31 -
      and that the assessments were accurate and complete. When licensee personnel
      performed emergent work, the inspectors verified that the licensee personnel promptly
      assessed and managed plant risk. The inspectors reviewed the scope of maintenance
      work, discussed the results of the assessment with the licensee's probabilistic risk
      analyst or shift technical advisor, and verified plant conditions were consistent with the
Enclosure 2
      risk assessment. The inspectors also reviewed the technical specification requirements
The inspectors selected these activities based on potential risk significance relative to  
      and inspected portions of redundant safety systems, when applicable, to verify risk
the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified  
      analysis assumptions were valid and applicable requirements were met. Specific
that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)  
      documents reviewed during this inspection are listed in the attachment.
and that the assessments were accurate and complete. When licensee personnel  
      These activities constitute completion of three maintenance risk assessments and
performed emergent work, the inspectors verified that the licensee personnel promptly  
      emergent work control inspection sample as defined by Inspection
assessed and managed plant risk. The inspectors reviewed the scope of maintenance  
      Procedure IP 71111.13-05.
work, discussed the results of the assessment with the licensee's probabilistic risk  
  b. Findings
analyst or shift technical advisor, and verified plant conditions were consistent with the  
.1   Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65(a)(4)
risk assessment. The inspectors also reviewed the technical specification requirements  
      involving the failure to adequately perform shutdown risk assessments during Refueling
and inspected portions of redundant safety systems, when applicable, to verify risk  
      Outage 17.
analysis assumptions were valid and applicable requirements were met. Specific  
      Description. While reviewing daily risk assessments during Refueling Outage 17, the
documents reviewed during this inspection are listed in the attachment.  
      inspectors noted discrepancies in the calculation of the risk conditions of the shutdown
These activities constitute completion of three maintenance risk assessments and  
      safety function condition. As a result, the inspectors reviewed the AP 22B-001, Outage
emergent work control inspection sample as defined by Inspection
      Risk Assessment, and Form APF 22B-001-02, Daily Shutdown Risk Assessment.
Procedure IP 71111.13-05.  
      Wolf Creek uses Procedure AP 22B-001, to implement the requirements of 10
b.  
      CFR 50.65(a)(4) during shutdown conditions (Modes 4, 5, 6, and defueled). In the
Findings  
      references section, the procedure lists NUMARC 93-01, Section 11, Assessment of
.1  
      Risk Resulting from Performance of Activities, as well as Regulatory Guide 1.182 in
Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65(a)(4)  
      which the NRC endorses NUMARC 93-01, Section 11, dated February 2000. Wolf
involving the failure to adequately perform shutdown risk assessments during Refueling  
      Creek has no NRC approved exceptions to Regulatory Guide 1.182. NUMARC 93-01,
Outage 17.  
      Section 11.3.5, provides a scope of five key Shutdown Safety Functions: decay heat
Description. While reviewing daily risk assessments during Refueling Outage 17, the  
      removal capability, inventory control, electric power availability, reactivity control, and
inspectors noted discrepancies in the calculation of the risk conditions of the shutdown  
      containment. Sections 11.3.6.1 through 11.3.6.5 provide specifics for each shutdown
safety function condition. As a result, the inspectors reviewed the AP 22B-001, Outage  
      function. Overall, the inspectors found several examples in which the five aspects
Risk Assessment, and Form APF 22B-001-02, Daily Shutdown Risk Assessment.
      NUMARC 93-01, Section 11, were not correctly implemented for risk assessments.
Wolf Creek uses Procedure AP 22B-001, to implement the requirements of 10  
      Form APF 22B-001-02 defines Condition 3 or High Risk as only one safety train is
CFR 50.65(a)(4) during shutdown conditions (Modes 4, 5, 6, and defueled). In the  
      available to satisfy the shutdown safety function. In the examples below, this
references section, the procedure lists NUMARC 93-01, Section 11, Assessment of  
      contradicted with Wolf Creeks actions.
Risk Resulting from Performance of Activities, as well as Regulatory Guide 1.182 in  
      For the Decay Heat Removal Shutdown Safety Function, Procedure APF 22B-001-02
which the NRC endorses NUMARC 93-01, Section 11, dated February 2000. Wolf  
      did not direct consideration of containment closure time per NUMARC 93-01,
Creek has no NRC approved exceptions to Regulatory Guide 1.182. NUMARC 93-01,  
      Section 11.3.6.1. The inspectors cross-referenced the daily shutdown risk assessment
Section 11.3.5, provides a scope of five key Shutdown Safety Functions: decay heat  
      forms with the equipment out-of-service list maintained in the control room log and found
removal capability, inventory control, electric power availability, reactivity control, and  
      three such instances of this occurring. First, on October 16 and 17, 2009, during the
containment. Sections 11.3.6.1 through 11.3.6.5 provide specifics for each shutdown  
                                          - 31 -                                    Enclosure 2
function. Overall, the inspectors found several examples in which the five aspects  
NUMARC 93-01, Section 11, were not correctly implemented for risk assessments.
Form APF 22B-001-02 defines Condition 3 or High Risk as only one safety train is  
available to satisfy the shutdown safety function. In the examples below, this  
contradicted with Wolf Creeks actions.  
For the Decay Heat Removal Shutdown Safety Function, Procedure APF 22B-001-02  
did not direct consideration of containment closure time per NUMARC 93-01,  
Section 11.3.6.1. The inspectors cross-referenced the daily shutdown risk assessment  
forms with the equipment out-of-service list maintained in the control room log and found  
three such instances of this occurring. First, on October 16 and 17, 2009, during the  


core offload, the reactor building equipment hatch was listed as closed during fuel
movement; however, the equipment out-of-service list showed the equipment hatch as
open from October 10 through November 15, 2009. Secondly, from October 14-17,
- 32 -
2009, and again on November 5-11, 2009, the reactor building auxiliary access hatch
was on the equipment out-of-service list because the interlocks were defeated to install
a temporary closure device. The daily risk assessment did not analyze this condition
which had the potential to impact the outcome of the risk assessment. The third
instance occurred on November 16, 2009, when the reactor building personnel hatch
Enclosure 2
failed to meet the surveillance requirement acceptance criteria. This was also not
core offload, the reactor building equipment hatch was listed as closed during fuel  
analyzed for its effect on containment closure.
movement; however, the equipment out-of-service list showed the equipment hatch as  
For the (Electric) Power Availability Shutdown Safety Function,
open from October 10 through November 15, 2009. Secondly, from October 14-17,  
Procedure APF 22B-001-02 did not explicitly direct consideration of ac and dc
2009, and again on November 5-11, 2009, the reactor building auxiliary access hatch  
instrumentation and control power availability per NUMARC 93-01, Section 11.3.6.3.
was on the equipment out-of-service list because the interlocks were defeated to install  
The inspectors cross-referenced the daily shutdown risk assessment forms with the
a temporary closure device. The daily risk assessment did not analyze this condition  
equipment out-of-service list maintained in the control room log archive and found two
which had the potential to impact the outcome of the risk assessment. The third  
such instances of this occurring. First from October 19 through 25, 2009, the 125Vdc
instance occurred on November 16, 2009, when the reactor building personnel hatch  
60-Cell Battery 4 was inoperable pending further analysis due to positive plate material
failed to meet the surveillance requirement acceptance criteria. This was also not  
separation identified during a visual inspection. The corresponding NK04 electrical bus
analyzed for its effect on containment closure.  
was incorrectly considered available on the six daily risk assessments performed during
For the (Electric) Power Availability Shutdown Safety Function,  
that time period. The second instance occurred on November 6 through 10, 2009, when
Procedure APF 22B-001-02 did not explicitly direct consideration of ac and dc  
the 125Vdc 60-Cell Battery 3 inoperable pending further analysis due to several cell
instrumentation and control power availability per NUMARC 93-01, Section 11.3.6.3.
abnormalities identified during a visual inspection. The corresponding NK03 electrical
The inspectors cross-referenced the daily shutdown risk assessment forms with the  
bus was incorrectly considered available on the five daily risk assessments performed
equipment out-of-service list maintained in the control room log archive and found two  
during that time period. Furthermore, these dc power unavailabilities were listed on the
such instances of this occurring. First from October 19 through 25, 2009, the 125Vdc  
risk assessment, but were not factored into its outcome (or color).
60-Cell Battery 4 was inoperable pending further analysis due to positive plate material  
For the Containment Shutdown Safety Function, Procedure APF 22B-001-02 did not
separation identified during a visual inspection. The corresponding NK04 electrical bus  
direct consideration of the availability of ventilation and radiation monitoring equipment
was incorrectly considered available on the six daily risk assessments performed during  
with respect to the filtration and monitoring of releases per NUMARC 93-01,
that time period. The second instance occurred on November 6 through 10, 2009, when  
Section 11.3.6.5. The inspectors again cross-referenced the daily shutdown risk
the 125Vdc 60-Cell Battery 3 inoperable pending further analysis due to several cell  
assessment forms with the equipment out-of-service list maintained in the control room
abnormalities identified during a visual inspection. The corresponding NK03 electrical  
log and identified two such instances of this occurring. The first instance occurred
bus was incorrectly considered available on the five daily risk assessments performed  
during core offload on October 17, 2009. At that time, the availability of Containment
during that time period. Furthermore, these dc power unavailabilities were listed on the  
Atmospheric Radiation Monitor GTRE0031 was degraded because it was being powered
risk assessment, but were not factored into its outcome (or color).  
by temporary power. The normal source, safety bus NB02, was de-energized for
For the Containment Shutdown Safety Function, Procedure APF 22B-001-02 did not  
maintenance from October 17 through 25, 2009. The second instance occurred during
direct consideration of the availability of ventilation and radiation monitoring equipment  
core reload on November 5 and 6, 2009, when the GTRE0021B was removed from
with respect to the filtration and monitoring of releases per NUMARC 93-01,  
service from October 29 through November 28, 2009, per the equipment out-of-service
Section 11.3.6.5. The inspectors again cross-referenced the daily shutdown risk  
list. Neither of these components was listed in the daily risk assessment, nor was their
assessment forms with the equipment out-of-service list maintained in the control room  
impact quantified in the determination of the risk level (or color).
log and identified two such instances of this occurring. The first instance occurred  
For the Decay Heat Removal Shutdown Safety Function, only residual heat removal
during core offload on October 17, 2009. At that time, the availability of Containment  
and steam generators can actually perform the function of heat removal. The risk
Atmospheric Radiation Monitor GTRE0031 was degraded because it was being powered  
assessments credited reactor cavity level greater than 23 feet above the vessel flange
by temporary power. The normal source, safety bus NB02, was de-energized for  
and a greater than 4-hour time to boil in the decay heat removal function. Thus, this
maintenance from October 17 through 25, 2009. The second instance occurred during  
configuration would be a permissible, moderate risk condition even if there were no
core reload on November 5 and 6, 2009, when the GTRE0021B was removed from  
active means of removing heat from the reactor. The inspectors cross-referenced the
service from October 29 through November 28, 2009, per the equipment out-of-service  
                                    - 32 -                                    Enclosure 2
list. Neither of these components was listed in the daily risk assessment, nor was their  
impact quantified in the determination of the risk level (or color).  
For the Decay Heat Removal Shutdown Safety Function, only residual heat removal  
and steam generators can actually perform the function of heat removal. The risk  
assessments credited reactor cavity level greater than 23 feet above the vessel flange  
and a greater than 4-hour time to boil in the decay heat removal function. Thus, this  
configuration would be a permissible, moderate risk condition even if there were no  
active means of removing heat from the reactor. The inspectors cross-referenced the  


  daily shutdown risk assessment forms with the equipment out-of-service list and
   
identified two instances of this occurring. First, on October 10, 2009 at 10:29 a.m., and
again on November 13 through 17, 2009, the risk assessments specified that steam
- 33 -
generators were available for heat removal when the auxiliary feedwater system was
unavailable because its safety-related water source (essential service water) was
isolated by Clearance Order C17-R-OP-S-005. Steam generators were available for
reflux cooling. Wolf Creek credits reflux cooling using EPRI Technical Report 102972,
Reflux Cooling: Application to Decay Heat Removal During Shutdown Operations.
Enclosure 2
The earliest EPRI analyzed scenario is 24 hours after shutdown; however, on
daily shutdown risk assessment forms with the equipment out-of-service list and  
October 10, 2009, only 10.5 hours following shutdown, the decay heat load would be
identified two instances of this occurring. First, on October 10, 2009 at 10:29 a.m., and  
significantly higher and warrant further analysis. The inspectors concluded that since
again on November 13 through 17, 2009, the risk assessments specified that steam  
this condition was unanalyzed, it could not be credited and a steam generator feedwater
generators were available for heat removal when the auxiliary feedwater system was  
source would be required for such a short time after reactor shutdown. The decay heat
unavailable because its safety-related water source (essential service water) was  
removal Shutdown Safety Function was categorized as normal risk (green) when it
isolated by Clearance Order C17-R-OP-S-005. Steam generators were available for  
should have been moderate risk (yellow) for the two risk assessments performed on
reflux cooling. Wolf Creek credits reflux cooling using EPRI Technical Report 102972,  
October 10, 2009. The other risk assessments that use reflux cooling were bounded by
Reflux Cooling: Application to Decay Heat Removal During Shutdown Operations.
the EPRI analysis. Lastly, the inspectors reviewed spent fuel pool cooling on
The earliest EPRI analyzed scenario is 24 hours after shutdown; however, on  
October 30, 2009. The risk assessment form specified one train was available and
October 10, 2009, only 10.5 hours following shutdown, the decay heat load would be  
resulted in moderate risk (yellow); however, red risk was defined as one safety train
significantly higher and warrant further analysis. The inspectors concluded that since  
available for the function. Although not an input to the color, the form specified normal
this condition was unanalyzed, it could not be credited and a steam generator feedwater  
and alternate makeup water sources to the spent fuel pool. Inspectors interviewed
source would be required for such a short time after reactor shutdown. The decay heat  
senior operators to identify the normal and alternate sources. One indicated that the
removal Shutdown Safety Function was categorized as normal risk (green) when it  
refueling water storage tank through the spent fuel pool transfer pumps was the normal
should have been moderate risk (yellow) for the two risk assessments performed on  
source. Another indicated demineralized water was the makeup source. For the
October 10, 2009. The other risk assessments that use reflux cooling were bounded by  
alternate makeup source, one indicated essential service water while another stated it
the EPRI analysis. Lastly, the inspectors reviewed spent fuel pool cooling on  
was fire water. In any case, none of the sources were specified and tracked by the risk
October 30, 2009. The risk assessment form specified one train was available and  
assessment form to mitigate the loss of one fuel pool cooling train.
resulted in moderate risk (yellow); however, red risk was defined as one safety train  
For the [Electric] Power Availability Shutdown Safety Function, a loss of offsite power,
available for the function. Although not an input to the color, the form specified normal  
or loss of both diesel generators, combined with no switchyard activities is categorized
and alternate makeup water sources to the spent fuel pool. Inspectors interviewed  
as a low risk condition. Furthermore, a station blackout with no switchyard activities in
senior operators to identify the normal and alternate sources. One indicated that the  
progress is a moderate risk condition. Inspectors found that this resulted in an
refueling water storage tank through the spent fuel pool transfer pumps was the normal  
inadequate risk assessment for electrical power in that the risk assessment would permit
source. Another indicated demineralized water was the makeup source. For the  
shutdown activities without any available sources of ac power. Wolf Creek categorized
alternate makeup source, one indicated essential service water while another stated it  
one in-service power source as moderate risk (yellow) rather than high risk. This was in
was fire water. In any case, none of the sources were specified and tracked by the risk  
contrast to the definition of high risk in which only one safety train available to satisfy the
assessment form to mitigate the loss of one fuel pool cooling train.  
function. The inspectors cross-referenced the daily shutdown risk assessment forms
For the [Electric] Power Availability Shutdown Safety Function, a loss of offsite power,  
with the equipment out-of-service list maintained in the control room log and found that
or loss of both diesel generators, combined with no switchyard activities is categorized  
on November 8, 2009, at 8:57 a.m. the risk assessment listed two diesel generators as
as a low risk condition. Furthermore, a station blackout with no switchyard activities in  
being available; however, the equipment out-of-service list indicated that emergency
progress is a moderate risk condition. Inspectors found that this resulted in an  
diesel generator A was out of service because essential service water train A was
inadequate risk assessment for electrical power in that the risk assessment would permit  
unavailable from November 5, 2009, at 4:37 a.m. until November 8, 2009, at 1:30 p.m.
shutdown activities without any available sources of ac power. Wolf Creek categorized  
When the credit for emergency diesel generator A is removed, the risk assessment
one in-service power source as moderate risk (yellow) rather than high risk. This was in  
outcome changes from normal risk (green) to moderate risk (yellow). The second
contrast to the definition of high risk in which only one safety train available to satisfy the  
instance occurred for the daily risk assessment performed between October 31 and
function. The inspectors cross-referenced the daily shutdown risk assessment forms  
November 4, 2009, which lists two diesel generators as being available. However, the
with the equipment out-of-service list maintained in the control room log and found that  
equipment out-of-service list indicated that emergency diesel generator B was out of
on November 8, 2009, at 8:57 a.m. the risk assessment listed two diesel generators as  
                                      - 33 -                                    Enclosure 2
being available; however, the equipment out-of-service list indicated that emergency  
diesel generator A was out of service because essential service water train A was  
unavailable from November 5, 2009, at 4:37 a.m. until November 8, 2009, at 1:30 p.m.
When the credit for emergency diesel generator A is removed, the risk assessment  
outcome changes from normal risk (green) to moderate risk (yellow). The second  
instance occurred for the daily risk assessment performed between October 31 and  
November 4, 2009, which lists two diesel generators as being available. However, the  
equipment out-of-service list indicated that emergency diesel generator B was out of  


  service because essential service water Train B was unavailable from October 16, 2009,
  at 10:05 p.m. until November 5, 2009, at 4:19 a.m. On all five daily risk assessments
  performed between October 31 and November 4, 2009, if the credit for the second diesel
- 34 -
  generator were removed, the outcome of the risk assessment changed from normal risk
  to moderate risk.
  Analysis. The failure to meet shutdown risk assessment requirements in the shutdown
  risk assessment process is a performance deficiency. Traditional enforcement does not
  apply since there were no actual safety consequences or potential for impacting the
Enclosure 2
  NRC's regulatory function, and the finding was not the result of any willful violation of
service because essential service water Train B was unavailable from October 16, 2009,  
  NRC requirements or Wolf Creek procedures. The inspectors determined that this
at 10:05 p.m. until November 5, 2009, at 4:19 a.m. On all five daily risk assessments  
  finding impacted the Mitigating Systems Cornerstone and was more than minor because
performed between October 31 and November 4, 2009, if the credit for the second diesel  
  it involved incorrect risk assessments that changed the outcome or color of the
generator were removed, the outcome of the risk assessment changed from normal risk  
  assessments. Per Inspection Manual Chapter 0609, Appendix K, Maintenance Risk
to moderate risk.  
  Assessment and Risk Management Significance Determination Process, licensees who
  only perform qualitative analyses of plant configuration risk due to maintenance
Analysis. The failure to meet shutdown risk assessment requirements in the shutdown  
  activities, the significance of the deficiencies must be determined by an internal NRC
risk assessment process is a performance deficiency. Traditional enforcement does not  
  management review using risk insights where possible in accordance with Inspection
apply since there were no actual safety consequences or potential for impacting the  
  Manual Chapter 612, Power Reactor Inspection Reports. The NRC management
NRC's regulatory function, and the finding was not the result of any willful violation of  
  review concluded that this finding was of Green safety significance because missing risk
NRC requirements or Wolf Creek procedures. The inspectors determined that this  
  management actions did not result in loss of key shutdown risk functions. Additionally,
finding impacted the Mitigating Systems Cornerstone and was more than minor because  
  the cause of the finding has a human performance crosscutting aspect in the area
it involved incorrect risk assessments that changed the outcome or color of the  
  associated with the resources. Specifically, Wolf Creek did not ensure that
assessments. Per Inspection Manual Chapter 0609, Appendix K, Maintenance Risk  
  Procedure APF 22B-001-02 was complete, accurate, and up-to-date [H.2(c)].
Assessment and Risk Management Significance Determination Process, licensees who  
  Enforcement. Title 10 CFR 50.65(a)(4) states, in part, that before performing
only perform qualitative analyses of plant configuration risk due to maintenance  
  maintenance activities (including but not limited to surveillance, postmaintenance testing,
activities, the significance of the deficiencies must be determined by an internal NRC  
  and corrective and preventive maintenance), the licensee shall assess and manage the
management review using risk insights where possible in accordance with Inspection  
  increase in risk that may result from the proposed maintenance activities. Contrary to
Manual Chapter 612, Power Reactor Inspection Reports. The NRC management  
  the above, between October 10, and November 17, 2009, Wolf Creek did not
review concluded that this finding was of Green safety significance because missing risk  
  appropriately assess and manage the increase in risk resulting from proposed
management actions did not result in loss of key shutdown risk functions. Additionally,  
  maintenance activities. Specifically, Form APF 22B-001-02 did not appropriately
the cause of the finding has a human performance crosscutting aspect in the area  
  consider electrical power, decay heat removal, and containment when assessing
associated with the resources. Specifically, Wolf Creek did not ensure that  
  shutdown risk. Because the finding is of very low safety significance and has been
Procedure APF 22B-001-02 was complete, accurate, and up-to-date [H.2(c)].  
  entered into the corrective action program as condition reports 22295 and 22296, this
Enforcement. Title 10 CFR 50.65(a)(4) states, in part, that before performing  
  violation is being treated as a noncited violation, consistent with Section VI.A of the NRC
maintenance activities (including but not limited to surveillance, postmaintenance testing,  
  Enforcement Policy: NCV 05000482/2009005-04, Failure to Incorporate Requirements
and corrective and preventive maintenance), the licensee shall assess and manage the  
  of Regulatory Guide 1.182 into Daily Shutdown Risk Assessments.
increase in risk that may result from the proposed maintenance activities. Contrary to  
.2 Introduction. On November 18, 2009, the inspectors identified a Green noncited
the above, between October 10, and November 17, 2009, Wolf Creek did not  
  violation of Technical Specification 3.0.4.b for ascension from Mode 4 to Mode 3 without
appropriately assess and manage the increase in risk resulting from proposed  
  establishing required risk management actions.
maintenance activities. Specifically, Form APF 22B-001-02 did not appropriately  
  Description. On the morning of November 18, 2009, the turbine-driven auxiliary
consider electrical power, decay heat removal, and containment when assessing  
  feedwater pump was inoperable per technical specification 3.0.4.b as specified in the
shutdown risk. Because the finding is of very low safety significance and has been  
  control room log at 11:53 p.m. the previous day upon ascension from Mode 4 into
entered into the corrective action program as condition reports 22295 and 22296, this  
  Mode 3 at 12:24 a.m. Technical specification 3.0.4.b permits mode ascension after
violation is being treated as a noncited violation, consistent with Section VI.A of the NRC  
  performance of a risk assessment to address the inoperable components and
Enforcement Policy: NCV 05000482/2009005-04, Failure to Incorporate Requirements  
                                        - 34 -                                  Enclosure 2
of Regulatory Guide 1.182 into Daily Shutdown Risk Assessments.  
.2  
Introduction. On November 18, 2009, the inspectors identified a Green noncited  
violation of Technical Specification 3.0.4.b for ascension from Mode 4 to Mode 3 without  
establishing required risk management actions.  
Description. On the morning of November 18, 2009, the turbine-driven auxiliary  
feedwater pump was inoperable per technical specification 3.0.4.b as specified in the  
control room log at 11:53 p.m. the previous day upon ascension from Mode 4 into  
Mode 3 at 12:24 a.m. Technical specification 3.0.4.b permits mode ascension after  
performance of a risk assessment to address the inoperable components and  


consideration and implementation of risk management actions to maintain safety in the
next mode. This condition is permissible for auxiliary feedwater per Technical
Specification LCO 3.7.5 so long as the ascension is below Mode 1. The entry was made
- 35 -
using an operational risk assessment Form APF 22C-003-01 in accordance with
Technical Specification LCO 3.0.4.b. The risk assessment on November 17, 2009,
specified:
1.       The turbine-driven auxiliary feedwater pump restoration following Surveillance
        Requirement 3.7.5.2, completion is expected within 48 hours of entering Mode 3.
Enclosure 2
2.       As a compensatory measure [risk management action], protected train signs
consideration and implementation of risk management actions to maintain safety in the  
        would be placed on the doors to the motor-driven auxiliary feedwater pumps A
next mode. This condition is permissible for auxiliary feedwater per Technical  
        and B room doors.
Specification LCO 3.7.5 so long as the ascension is below Mode 1. The entry was made  
A walkdown conducted by the inspector at 10:30 a.m. on November 18, 2009, found that
using an operational risk assessment Form APF 22C-003-01 in accordance with  
the protected train signs on the motor-driven auxiliary feedwater pump rooms specified
Technical Specification LCO 3.0.4.b. The risk assessment on November 17, 2009,  
by the operational risk assessment were not in place. Also, a maintenance crew was
specified:  
performing radiography in the motor-driven auxiliary feedwater pump Room B. A further
1.  
review of the control room logs revealed that motor-driven auxiliary feedwater pump
The turbine-driven auxiliary feedwater pump restoration following Surveillance  
comprehensive pump testing, flow path verification, and containment isolation valve
Requirement 3.7.5.2, completion is expected within 48 hours of entering Mode 3.  
verification testing were scheduled and performed, making both motor-driven auxiliary
2.  
feedwater pumps A and B inoperable (at separate times) during the morning of
As a compensatory measure [risk management action], protected train signs  
November 18, 2009, while turbine-driven auxiliary feedwater was still inoperable.
would be placed on the doors to the motor-driven auxiliary feedwater pumps A  
Operators did make proper entry into Technical Specification 3.7.5, Condition C, for two
and B room doors.  
of three auxiliary feedwater trains inoperable; however, this configuration was not
A walkdown conducted by the inspector at 10:30 a.m. on November 18, 2009, found that  
analyzed in the risk assessment. Immediately following the walkdown, the inspector
the protected train signs on the motor-driven auxiliary feedwater pump rooms specified  
discussed the issue with the shift manager, the protected train signs were installed on
by the operational risk assessment were not in place. Also, a maintenance crew was  
the motor-driven auxiliary feedwater pump room doors and a condition report was
performing radiography in the motor-driven auxiliary feedwater pump Room B. A further  
initiated. Wolf Creek determined that an informal mode ascension check off list was
review of the control room logs revealed that motor-driven auxiliary feedwater pump  
used that conflicted with the risk assessment performed for Technical
comprehensive pump testing, flow path verification, and containment isolation valve  
Specification 3.0.4.b.
verification testing were scheduled and performed, making both motor-driven auxiliary  
Analysis. Mode ascension under Technical Specification LCO 3.0.4.b without
feedwater pumps A and B inoperable (at separate times) during the morning of  
establishing required risk management actions is a performance deficiency. Traditional
November 18, 2009, while turbine-driven auxiliary feedwater was still inoperable.
enforcement does not apply since there were no actual safety consequences or potential
Operators did make proper entry into Technical Specification 3.7.5, Condition C, for two  
for impacting the NRC's regulatory function, and the finding was not the result of any
of three auxiliary feedwater trains inoperable; however, this configuration was not  
willful violation of NRC requirements or Wolf Creek procedures. The inspectors
analyzed in the risk assessment. Immediately following the walkdown, the inspector  
determined that the violation was more than minor because it was associated with the
discussed the issue with the shift manager, the protected train signs were installed on  
configuration control and alignment attribute of the Mitigating Systems Cornerstone and
the motor-driven auxiliary feedwater pump room doors and a condition report was  
affected the cornerstone objective to ensure the availability, reliability, and capability of
initiated. Wolf Creek determined that an informal mode ascension check off list was  
systems that respond to initiating events to prevent undesirable consequences. The
used that conflicted with the risk assessment performed for Technical  
configuration control issues not only included the work being completed on the
Specification 3.0.4.b.  
turbine-driven auxiliary feedwater pump, but also included containment isolation valve
Analysis. Mode ascension under Technical Specification LCO 3.0.4.b without  
testing and radiography that was performed on the motor-driven auxiliary feedwater
establishing required risk management actions is a performance deficiency. Traditional  
pumps which was not included in the risk assessment. The inspector used Inspection
enforcement does not apply since there were no actual safety consequences or potential  
Manual Chapter 0609.04, Phase 1 SDP - Worksheet, to determine that the finding was
for impacting the NRC's regulatory function, and the finding was not the result of any  
of very low safety significance (Green) because it did not result in a loss of system safety
willful violation of NRC requirements or Wolf Creek procedures. The inspectors  
function; exceed allowable technical specification outage time; and was not a seismic,
determined that the violation was more than minor because it was associated with the  
                                    - 35 -                                    Enclosure 2
configuration control and alignment attribute of the Mitigating Systems Cornerstone and  
affected the cornerstone objective to ensure the availability, reliability, and capability of  
systems that respond to initiating events to prevent undesirable consequences. The  
configuration control issues not only included the work being completed on the  
turbine-driven auxiliary feedwater pump, but also included containment isolation valve  
testing and radiography that was performed on the motor-driven auxiliary feedwater  
pumps which was not included in the risk assessment. The inspector used Inspection  
Manual Chapter 0609.04, Phase 1 SDP - Worksheet, to determine that the finding was  
of very low safety significance (Green) because it did not result in a loss of system safety  
function; exceed allowable technical specification outage time; and was not a seismic,  


  flooding, or severe weather concern. Additionally, the cause of the finding has a human
  performance crosscutting aspect in the area associated with the decision making.
  Specifically, Wolf Creek used a risk assessment form and informal mode change form to
- 36 -
  communicate between departments the requirement for risk management actions. The
  two forms were in conflict, and the personnel who implemented the risk management
  actions were not informed [H.1(c)].
  Enforcement. Wolf Creek Technical Specification LCO 3.0.4.b states, in part, When an
  LCO is not met, entry into a MODE or other specified condition in the Applicability shall
Enclosure 2
  only be made after performance of a risk assessment addressing inoperable systems
flooding, or severe weather concern. Additionally, the cause of the finding has a human  
  and components, consideration of the results, determination of the acceptability of
performance crosscutting aspect in the area associated with the decision making.
  entering the MODE or other specified condition in the Applicability, and establishment of
Specifically, Wolf Creek used a risk assessment form and informal mode change form to  
  risk management actions, if appropriate. Prior to MODE ascension with the
communicate between departments the requirement for risk management actions. The  
  turbine-driven auxiliary feedwater pump inoperable, Wolf Creek performed a risk
two forms were in conflict, and the personnel who implemented the risk management  
  assessment and identified risk management actions. Contrary to the above, on
actions were not informed [H.1(c)].  
  November 18, 2009, at 12:24 a.m. Wolf Creek invoked Technical Specification 3.0.4.b to
Enforcement. Wolf Creek Technical Specification LCO 3.0.4.b states, in part, When an  
  ascend from Mode 4 to Mode 3 without implementing the risk management actions
LCO is not met, entry into a MODE or other specified condition in the Applicability shall  
  required by the risk assessment performed to justify the Mode change with the
only be made after performance of a risk assessment addressing inoperable systems  
  turbine-driven auxiliary feedwater pump inoperable. Because the finding is of very low
and components, consideration of the results, determination of the acceptability of  
  safety significance and has been entered into the corrective action program as Condition
entering the MODE or other specified condition in the Applicability, and establishment of  
  Report 00021926, this violation is being treated as a noncited violation, consistent with
risk management actions, if appropriate. Prior to MODE ascension with the  
  Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-05, Mode
turbine-driven auxiliary feedwater pump inoperable, Wolf Creek performed a risk  
  Change under Technical Specification 3.0.4.b Without Required Risk Management
assessment and identified risk management actions. Contrary to the above, on  
  Actions.
November 18, 2009, at 12:24 a.m. Wolf Creek invoked Technical Specification 3.0.4.b to  
.3 Introduction. On October 15, 2009, the inspectors identified a violation of 10 CFR
ascend from Mode 4 to Mode 3 without implementing the risk management actions  
  Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to
required by the risk assessment performed to justify the Mode change with the  
  follow Procedure AP 28A-100, Condition Reports. Wolf Creek failed to initiate a
turbine-driven auxiliary feedwater pump inoperable. Because the finding is of very low  
  condition report for evaluation of corrosion on containment cooler A piping.
safety significance and has been entered into the corrective action program as Condition  
  Description. On October 15, 2009, the inspectors identified dried white and brown
Report 00021926, this violation is being treated as a noncited violation, consistent with  
  deposits on vertical piping from insulation seams on containment cooler A. The
Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-05, Mode  
  inspectors identified the condition to Wolf Creek. On October 17, Wolf Creek completed
Change under Technical Specification 3.0.4.b Without Required Risk Management  
  Work Order 09-321113-000 to remove the insulation and found significant corrosion of
Actions.  
  piping and flanges for containment cooler A. Work Order 09-321113-000 stated that the
.3  
  cause of the corrosion was unknown. Wolf Creek informed the inspectors that the cause
Introduction. On October 15, 2009, the inspectors identified a violation of 10 CFR  
  of the corrosion was condensation. The inspectors noted that since no ultrasonic testing
Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to  
  had been performed, leakage from through-wall defects could not be eliminated as a
follow Procedure AP 28A-100, Condition Reports. Wolf Creek failed to initiate a  
  cause. Wolf Creek later informed the inspectors that the visual inspection showed no
condition report for evaluation of corrosion on containment cooler A piping.  
  through wall defects. The inspectors again challenged Wolf Creek since no ultrasonic
Description. On October 15, 2009, the inspectors identified dried white and brown  
  testing was performed to demonstrate that through wall defects could be eliminated as a
deposits on vertical piping from insulation seams on containment cooler A. The  
  cause. The inspectors reviewed Procedure AP 28A-100, Condition Reports,
inspectors identified the condition to Wolf Creek. On October 17, Wolf Creek completed  
  Revision 10, Attachment C. Attachment C required condition reports when equipment
Work Order 09-321113-000 to remove the insulation and found significant corrosion of  
  issues require evaluation beyond the work controls (work order) process.
piping and flanges for containment cooler A. Work Order 09-321113-000 stated that the  
  Procedure AP 28A-100 defines an adverse condition as one that could impact nuclear
cause of the corrosion was unknown. Wolf Creek informed the inspectors that the cause  
  safety. Wolf Creek subsequently initiated Condition Report 20964 on October 21, 2009,
of the corrosion was condensation. The inspectors noted that since no ultrasonic testing  
  stating that there was extensive corrosion on containment cooler A and that all
had been performed, leakage from through-wall defects could not be eliminated as a  
  containment coolers could be affected. Condition Report 20964 went on to evaluate the
cause. Wolf Creek later informed the inspectors that the visual inspection showed no  
                                      - 36 -                                  Enclosure 2
through wall defects. The inspectors again challenged Wolf Creek since no ultrasonic  
testing was performed to demonstrate that through wall defects could be eliminated as a  
cause. The inspectors reviewed Procedure AP 28A-100, Condition Reports,  
Revision 10, Attachment C. Attachment C required condition reports when equipment  
issues require evaluation beyond the work controls (work order) process.
Procedure AP 28A-100 defines an adverse condition as one that could impact nuclear  
safety. Wolf Creek subsequently initiated Condition Report 20964 on October 21, 2009,  
stating that there was extensive corrosion on containment cooler A and that all  
containment coolers could be affected. Condition Report 20964 went on to evaluate the  


piping insulation and how it did not prevent condensation on the piping which allowed
the corrosion.
On October 23 and October 26, Wolf Creek initiated several work requests to perform
- 37 -
ultrasonic testing of containment coolers A, B, and C. Wolf Creek initiated the work
order to perform piping and flange thickness measurements which were found to be
satisfactory. Wolf Creek engineering determined that containment coolers A, B, and C
had piping flange studs that needed to be replaced due to corrosion. From November 1
to November 2, a total of 32 studs and 96 nuts were replaced for the three coolers. On
Enclosure 2
November 8 and 11, 2009, Wolf Creek completed engineering dispositions to address
piping insulation and how it did not prevent condensation on the piping which allowed  
the cause and the results of the ultrasonic testing. Condition Report 22443 also
the corrosion.  
identified the need for more ultrasonic inspections in the next refueling outage to verify
On October 23 and October 26, Wolf Creek initiated several work requests to perform  
acceptable corrosion rates. On December 16, 2009, Wolf Creek initiated Condition
ultrasonic testing of containment coolers A, B, and C. Wolf Creek initiated the work  
Report 22443 which described the lack of a timely condition report to determine a cause
order to perform piping and flange thickness measurements which were found to be  
of the corrosion.
satisfactory. Wolf Creek engineering determined that containment coolers A, B, and C  
Analysis. The inspectors determined that the failure to follow Procedure AP 28A-100,
had piping flange studs that needed to be replaced due to corrosion. From November 1  
Appendix C, was a performance deficiency. Traditional enforcement does not apply
to November 2, a total of 32 studs and 96 nuts were replaced for the three coolers. On  
since there were no actual safety consequences or potential for impacting the NRCs
November 8 and 11, 2009, Wolf Creek completed engineering dispositions to address  
regulatory function, and the finding was not the result of any willful violation of NRC
the cause and the results of the ultrasonic testing. Condition Report 22443 also  
requirements or Wolf Creek procedures. This issue was more than minor because it
identified the need for more ultrasonic inspections in the next refueling outage to verify  
was associated with the equipment performance attribute of the Mitigating Systems
acceptable corrosion rates. On December 16, 2009, Wolf Creek initiated Condition  
Cornerstone and affected the cornerstone objective to ensure the availability, reliability,
Report 22443 which described the lack of a timely condition report to determine a cause  
and capability of systems that respond to initiating events to prevent undesirable
of the corrosion.  
consequences. Using Inspection Manual Chapter 0609.04, the issue screened to Green
Analysis. The inspectors determined that the failure to follow Procedure AP 28A-100,  
because there was not a loss of operability and the finding did not screen as potentially
Appendix C, was a performance deficiency. Traditional enforcement does not apply  
risk significant due to a seismic, flooding, or severe weather initiating event. A
since there were no actual safety consequences or potential for impacting the NRCs  
crosscutting aspect was identified in the problem identification and resolution area of the
regulatory function, and the finding was not the result of any willful violation of NRC  
corrective action program. Specifically, Wolf Creek failed to implement a corrective
requirements or Wolf Creek procedures. This issue was more than minor because it  
action program with a low threshold for identifying issues [P.1.a].
was associated with the equipment performance attribute of the Mitigating Systems  
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
Cornerstone and affected the cornerstone objective to ensure the availability, reliability,  
and Drawings, requires, in part, that activities affecting quality be described by
and capability of systems that respond to initiating events to prevent undesirable  
documented instructions, procedures or drawings appropriate to the circumstances and
consequences. Using Inspection Manual Chapter 0609.04, the issue screened to Green  
be accomplished in accordance with these instructions, procedures or drawings.
because there was not a loss of operability and the finding did not screen as potentially  
Procedure AP 28A-100, Attachment C, Equipment Problems Requiring a Condition
risk significant due to a seismic, flooding, or severe weather initiating event. A  
Report, requires, in part, that condition reports be written where further evaluation is
crosscutting aspect was identified in the problem identification and resolution area of the  
needed outside the work control process. Contrary to the above, from October 15 to 23,
corrective action program. Specifically, Wolf Creek failed to implement a corrective  
2009, Wolf Creek failed to complete an activity affecting quality in accordance with
action program with a low threshold for identifying issues [P.1.a].  
documented procedures appropriate to the circumstances. Specifically, Wolf Creek
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
failed to write a condition report for corrosion on containment cooler A after Work
and Drawings, requires, in part, that activities affecting quality be described by  
Order 09-321113-000 stated that the cause of the corrosion was unknown. Because this
documented instructions, procedures or drawings appropriate to the circumstances and  
violation was determined to be of very low safety significance and was placed in the
be accomplished in accordance with these instructions, procedures or drawings.
corrective action program as Condition Reports 20964 and 22443, this violation is being
Procedure AP 28A-100, Attachment C, Equipment Problems Requiring a Condition  
treated as a noncited violation in accordance with Section VI.A.1 of the Enforcement
Report, requires, in part, that condition reports be written where further evaluation is  
Policy: NCV 05000482/2009005-06, Failure to Follow Corrective Action Procedure.
needed outside the work control process. Contrary to the above, from October 15 to 23,  
                                      - 37 -                                  Enclosure 2
2009, Wolf Creek failed to complete an activity affecting quality in accordance with  
documented procedures appropriate to the circumstances. Specifically, Wolf Creek  
failed to write a condition report for corrosion on containment cooler A after Work  
Order 09-321113-000 stated that the cause of the corrosion was unknown. Because this  
violation was determined to be of very low safety significance and was placed in the  
corrective action program as Condition Reports 20964 and 22443, this violation is being  
treated as a noncited violation in accordance with Section VI.A.1 of the Enforcement  
Policy: NCV 05000482/2009005-06, Failure to Follow Corrective Action Procedure.  


.4 Introduction. On November 23, 2009, a self-revealing violation of Technical
  Specification 5.4.1.a was reviewed by the inspectors after a technician failed to follow
  procedures and emptied 45 gallons of oil from centrifugal charging pump A.
- 38 -
  Description. On November, 23, 2009, a technician loosened the wrong nut and removed
  the thermowell for Temperature Indicator BG TI-0036 on centrifugal charging pump A. At
  the time, the auxiliary lube oil pump was running. The auxiliary lube oil pump normally
  runs while the pump is in standby. This emptied 45 gallons of oil from the pump.
  Removal of the temperature indicator normally would not affect operability since the oil
Enclosure 2
  temperature indication is not required; however, the pump cannot function without lube
.4  
  oil. Control room operators declared the pump inoperable and entered Technical
Introduction. On November 23, 2009, a self-revealing violation of Technical  
  Specification 3.5.2. Approximately 10 hours later, the thermowell and oil were replaced,
Specification 5.4.1.a was reviewed by the inspectors after a technician failed to follow  
  the pump was leak tested and Technical Specification 3.5.2, Condition A was exited.
procedures and emptied 45 gallons of oil from centrifugal charging pump A.  
  Wolf Creek performed a root cause analysis for this issue under Condition
Description. On November, 23, 2009, a technician loosened the wrong nut and removed  
  Report 21993. During interviews, the technician stated that he performed a 2 minute
the thermowell for Temperature Indicator BG TI-0036 on centrifugal charging pump A. At  
  self-check (a recognized error reduction technique at Wolf Creek) but failed to identify
the time, the auxiliary lube oil pump was running. The auxiliary lube oil pump normally  
  the correct nut to loosen. This task is a required training task for these temperature
runs while the pump is in standby. This emptied 45 gallons of oil from the pump.
  indicators, which involves a similar training rig. The technician stated that he understood
Removal of the temperature indicator normally would not affect operability since the oil  
  the difference between the thermowell nut and the temperature indicator but failed to
temperature indication is not required; however, the pump cannot function without lube  
  make the differentiation on November 23. The technician and the supervisor discussed
oil. Control room operators declared the pump inoperable and entered Technical  
  the work, but the communication was inadequate because the technician was left with
Specification 3.5.2. Approximately 10 hours later, the thermowell and oil were replaced,  
  the idea to perform the work independently, and the supervisor believed that the
the pump was leak tested and Technical Specification 3.5.2, Condition A was exited.  
  technician was only going to perform a walkdown of the indicator. The prejob briefing
Wolf Creek performed a root cause analysis for this issue under Condition  
  standard at Wolf Creek required supervisor approval for a self-briefing.
Report 21993.   During interviews, the technician stated that he performed a 2 minute  
  Analysis. The failure to follow Procedure STN IC-294A and correctly remove the
self-check (a recognized error reduction technique at Wolf Creek) but failed to identify  
  detector was considered a performance deficiency. Traditional enforcement does not
the correct nut to loosen. This task is a required training task for these temperature  
  apply since there were no actual safety consequences or potential for impacting the
indicators, which involves a similar training rig. The technician stated that he understood  
  NRC's regulatory function, and the finding was not the result of any willful violation of
the difference between the thermowell nut and the temperature indicator but failed to  
  NRC requirements or Wolf Creek procedures. The finding was more than minor
make the differentiation on November 23. The technician and the supervisor discussed  
  because it was associated with the equipment performance attribute of the Mitigating
the work, but the communication was inadequate because the technician was left with  
  Systems Cornerstone, and it affected the cornerstone objective to ensure the availability,
the idea to perform the work independently, and the supervisor believed that the  
  reliability, and capability of systems that respond to initiating events to prevent
technician was only going to perform a walkdown of the indicator. The prejob briefing  
  undesirable consequences. The inspectors evaluated the significance of this finding
standard at Wolf Creek required supervisor approval for a self-briefing.  
  using Phase 1 of Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and
Analysis. The failure to follow Procedure STN IC-294A and correctly remove the  
  Characterization of Findings, and determined that the finding was of very low safety
detector was considered a performance deficiency. Traditional enforcement does not  
  significance (Green) because the pump was inoperable for less than 24 hours. Also, the
apply since there were no actual safety consequences or potential for impacting the  
  finding did not screen as potentially risk significant due to a seismic, flooding, or severe
NRC's regulatory function, and the finding was not the result of any willful violation of  
  weather initiating event. The inspectors identified a human performance crosscutting in
NRC requirements or Wolf Creek procedures. The finding was more than minor  
  the area of work practices because a 2-minute self-check and communication with the
because it was associated with the equipment performance attribute of the Mitigating  
  supervisor failed to prevent the event [H.4.a].
Systems Cornerstone, and it affected the cornerstone objective to ensure the availability,  
  Enforcement. Technical Specification 5.4.1.a requires the implementation of written
reliability, and capability of systems that respond to initiating events to prevent  
  procedures described in Regulatory Guide 1.33, Revision 2, Appendix A. Section 9.A of
undesirable consequences. The inspectors evaluated the significance of this finding  
  Regulatory Guide 1.33 requires procedures for performing maintenance that can affect
using Phase 1 of Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and  
  the performance of safety-related equipment. Procedure STN IC-294A, Calibration of
Characterization of Findings, and determined that the finding was of very low safety  
  CCP A Outboard Bearing and Lube Oil Supply Temperature Indicators BGTI0036
significance (Green) because the pump was inoperable for less than 24 hours. Also, the  
                                        - 38 -                                    Enclosure 2
finding did not screen as potentially risk significant due to a seismic, flooding, or severe  
weather initiating event. The inspectors identified a human performance crosscutting in  
the area of work practices because a 2-minute self-check and communication with the  
supervisor failed to prevent the event [H.4.a].  
Enforcement. Technical Specification 5.4.1.a requires the implementation of written  
procedures described in Regulatory Guide 1.33, Revision 2, Appendix A. Section 9.A of  
Regulatory Guide 1.33 requires procedures for performing maintenance that can affect  
the performance of safety-related equipment. Procedure STN IC-294A, Calibration of  
CCP A Outboard Bearing and Lube Oil Supply Temperature Indicators BGTI0036  


      and BGTI0040, Revision 0, step 8.2.1, requires that the temperature detector be
      removed from its thermowell for calibration. Contrary to the above, on November 23,
      2009, a worker removed the thermowell and breached the lube oil subsystem. Because
- 39 -
      this violation was determined to be of very low safety significance and was placed in the
      corrective action program as Condition Report 21993, this violation is being treated as a
      noncited violation in accordance with Section VI.A.1 of the Enforcement Policy:
      NCV 05000482/2009005-07, Failure to Follow Procedure Results in Draining of
      Emergency Core Cooling System Pump Oil.
Enclosure 2
1R15 Operability Evaluations (71111.15)
and BGTI0040, Revision 0, step 8.2.1, requires that the temperature detector be  
  a. Inspection Scope
removed from its thermowell for calibration. Contrary to the above, on November 23,  
      The inspectors reviewed the following issues:
2009, a worker removed the thermowell and breached the lube oil subsystem. Because  
      *       October 9, 2009, Source range nuclear instrument (NI)-31 response
this violation was determined to be of very low safety significance and was placed in the  
      *       November 5, 2009, Essential service water pump seismic operability
corrective action program as Condition Report 21993, this violation is being treated as a  
      The inspectors selected these potential operability issues based on the risk-significance
noncited violation in accordance with Section VI.A.1 of the Enforcement Policy:  
      of the associated components and systems. The inspectors evaluated the technical
NCV 05000482/2009005-07, Failure to Follow Procedure Results in Draining of  
      adequacy of the evaluations to ensure that technical specification operability was
Emergency Core Cooling System Pump Oil.  
      properly justified and the subject component or system remained available such that no
1R15 Operability Evaluations (71111.15)  
      unrecognized increase in risk occurred. The inspectors compared the operability and
a.  
      design criteria in the appropriate sections of the technical specifications and USAR to
Inspection Scope  
      the licensees evaluations, to determine whether the components or systems were
The inspectors reviewed the following issues:  
      operable. Where compensatory measures were required to maintain operability, the
*  
      inspectors determined whether the measures in place would function as intended and
October 9, 2009, Source range nuclear instrument (NI)-31 response  
      were properly controlled. The inspectors determined, where appropriate, compliance
*  
      with bounding limitations associated with the evaluations. Additionally, the inspectors
November 5, 2009, Essential service water pump seismic operability  
      also reviewed a sampling of corrective action documents to verify that the licensee was
      identifying and correcting any deficiencies associated with operability evaluations.
The inspectors selected these potential operability issues based on the risk-significance  
      Specific documents reviewed during this inspection are listed in the attachment.
of the associated components and systems. The inspectors evaluated the technical  
      These activities constitute completion of three operability evaluations inspection samples
adequacy of the evaluations to ensure that technical specification operability was  
      as defined in Inspection Procedure IP 71111.15-05
properly justified and the subject component or system remained available such that no  
  b. Findings
unrecognized increase in risk occurred. The inspectors compared the operability and  
.1   Introduction. On November 5, 2009, the inspectors identified a Green noncited violation
design criteria in the appropriate sections of the technical specifications and USAR to  
      of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,
the licensees evaluations, to determine whether the components or systems were  
      for failure to perform an adequate operability evaluation as required by procedure.
operable. Where compensatory measures were required to maintain operability, the  
      Description. On November 1, 2009, Wolf Creek was defueled for Refueling Outage 17,
inspectors determined whether the measures in place would function as intended and  
      and essential service water pump A was being replaced. On November 1, 2009, Wolf
were properly controlled. The inspectors determined, where appropriate, compliance  
      Creek found that the as-constructed clearances at the essential service water pump A
with bounding limitations associated with the evaluations. Additionally, the inspectors  
      flange did not meet design requirements. This allowed the pump column to flex up to
also reviewed a sampling of corrective action documents to verify that the licensee was  
      0.125 inches until it would engage the seismic supports. The pumps were designed to
identifying and correcting any deficiencies associated with operability evaluations.
      be rigidly restrained. This resulted in Condition Reports 21400 and 21572. Wolf Creek
Specific documents reviewed during this inspection are listed in the attachment.  
                                          - 39 -                                    Enclosure 2
These activities constitute completion of three operability evaluations inspection samples  
as defined in Inspection Procedure IP 71111.15-05  
b.  
Findings  
.1  
Introduction. On November 5, 2009, the inspectors identified a Green noncited violation  
of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,  
for failure to perform an adequate operability evaluation as required by procedure.  
Description. On November 1, 2009, Wolf Creek was defueled for Refueling Outage 17,  
and essential service water pump A was being replaced. On November 1, 2009, Wolf  
Creek found that the as-constructed clearances at the essential service water pump A  
flange did not meet design requirements. This allowed the pump column to flex up to  
0.125 inches until it would engage the seismic supports. The pumps were designed to  
be rigidly restrained. This resulted in Condition Reports 21400 and 21572. Wolf Creek  


completed Operability Evaluation EF-09-010 that provided the basis for the past
operability of essential service water Pump A and future operability of essential service
water pump B on November 1, 2009, and initiated Condition Report 22400 to correct the
- 40 -
clearances.
On November 5, 2009, the inspectors reviewed Operability Evaluation EF-09-010. The
evaluation concluded that the increased movement of the pump would increase stresses
to 10 ksi, which was below the specified allowable ASME Code Section III limit of
17.5 ksi. The evaluation identified requirements that the pumps shall operate during and
Enclosure 2
after a safe shutdown earthquake as one of the design basis functions as required per
completed Operability Evaluation EF-09-010 that provided the basis for the past  
10 CFR Part 50, Appendix A, General Design Criterion 2. These seismic design
operability of essential service water Pump A and future operability of essential service  
requirements are contained in Sections 3.9(B) and 9.2.1 of the USAR. The inspectors
water pump B on November 1, 2009, and initiated Condition Report 22400 to correct the  
found that the operability evaluations technical basis was inadequate due to the
clearances.  
following: (1) the evaluation did not contain a formal calculation that demonstrated that
On November 5, 2009, the inspectors reviewed Operability Evaluation EF-09-010. The  
stresses were below limits, (2) the evaluation only considered operating basis
evaluation concluded that the increased movement of the pump would increase stresses  
earthquake accelerations and not the larger safe shutdown earthquake accelerations,
to 10 ksi, which was below the specified allowable ASME Code Section III limit of  
(3) the evaluation did not contain a calculation to demonstrate that the pump impeller
17.5 ksi. The evaluation identified requirements that the pumps shall operate during and  
clearances were allowable if an earthquake occurred while the pump was running, and
after a safe shutdown earthquake as one of the design basis functions as required per  
(4) the method of analysis for the stresses was not described as an appropriate
10 CFR Part 50, Appendix A, General Design Criterion 2. These seismic design  
alternative method to the original stress calculation done with the SAP V computer
requirements are contained in Sections 3.9(B) and 9.2.1 of the USAR. The inspectors  
program. The inspectors could not verify that the simplified method was appropriate.
found that the operability evaluations technical basis was inadequate due to the  
The inspectors reviewed Procedure AP 26C-004, Technical Specification Operability,
following: (1) the evaluation did not contain a formal calculation that demonstrated that  
Revision 20 and Procedure AP 28-001, Operability Evaluations, Revision 17.
stresses were below limits, (2) the evaluation only considered operating basis  
Procedure AP 26C-004, step 6.2.6, states that documentation for prompt operability
earthquake accelerations and not the larger safe shutdown earthquake accelerations,  
evaluations shall include information needed to support operability. Step 4.5 states that
(3) the evaluation did not contain a calculation to demonstrate that the pump impeller  
safety functions specified in the current licensing basis shall be met.
clearances were allowable if an earthquake occurred while the pump was running, and  
Procedure AP 28-001, Operability Evaluations, step 4.9, also describes that the
(4) the method of analysis for the stresses was not described as an appropriate  
specified safety functions in the current licensing basis shall be met. Step 6.1.7 states
alternative method to the original stress calculation done with the SAP V computer  
that design basis events and safety evaluations should be considered. There is no
program. The inspectors could not verify that the simplified method was appropriate.  
description of the use of alternative analysis methods in AP 28-001 or AP 26C-004 that
The inspectors reviewed Procedure AP 26C-004, Technical Specification Operability,  
is consistent with Regulatory Information Summary 2005-20, Section C.4.
Revision 20 and Procedure AP 28-001, Operability Evaluations, Revision 17.
On November 7, 2009, Wolf Creek initiated Condition Report 21572 to resolve the items
Procedure AP 26C-004, step 6.2.6, states that documentation for prompt operability  
identified above. Wolf Creek completed Operability Evaluation EF-09-010, Revision 1,
evaluations shall include information needed to support operability. Step 4.5 states that  
on December 14, 2009. The inspectors reviewed Revision 1 and determined the above
safety functions specified in the current licensing basis shall be met.
identified deficiencies still existed. Wolf Creek performed a third revision to Operability
Procedure AP 28-001, Operability Evaluations, step 4.9, also describes that the  
Evaluation EF-09-010 and initiated Condition Report 22798. The four items were
specified safety functions in the current licensing basis shall be met. Step 6.1.7 states  
resolved with Operability Evaluation EF-09-010, Revision 2 which contained drawings
that design basis events and safety evaluations should be considered. There is no  
and calculations to demonstrate that the pumps were seismically qualified and that the
description of the use of alternative analysis methods in AP 28-001 or AP 26C-004 that  
simplified calculations were appropriate. In Revision 2, the calculated stresses
is consistent with Regulatory Information Summary 2005-20, Section C.4.  
increased to 16.4 ksi but were still below the limit of 17.5 ksi.
On November 7, 2009, Wolf Creek initiated Condition Report 21572 to resolve the items  
Analysis. The failure to perform an adequate operability evaluation per
identified above. Wolf Creek completed Operability Evaluation EF-09-010, Revision 1,  
Procedures AP 28-001 and AP 26C-004, was a performance deficiency. Traditional
on December 14, 2009. The inspectors reviewed Revision 1 and determined the above  
enforcement does not apply since there were no actual safety consequences or potential
identified deficiencies still existed. Wolf Creek performed a third revision to Operability  
for impacting the NRC's regulatory function, and the finding was not the result of any
Evaluation EF-09-010 and initiated Condition Report 22798. The four items were  
willful violation of NRC requirements or Wolf Creek procedures. The inspectors
resolved with Operability Evaluation EF-09-010, Revision 2 which contained drawings  
                                      - 40 -                                  Enclosure 2
and calculations to demonstrate that the pumps were seismically qualified and that the  
simplified calculations were appropriate. In Revision 2, the calculated stresses  
increased to 16.4 ksi but were still below the limit of 17.5 ksi.  
Analysis. The failure to perform an adequate operability evaluation per  
Procedures AP 28-001 and AP 26C-004, was a performance deficiency. Traditional  
enforcement does not apply since there were no actual safety consequences or potential  
for impacting the NRC's regulatory function, and the finding was not the result of any  
willful violation of NRC requirements or Wolf Creek procedures. The inspectors  


  determined that this finding was more than minor because it is associated with the
  equipment performance attribute for the Mitigating Systems Cornerstone, and it affected
  the cornerstone objective to ensure the availability, reliability, and capability of systems
- 41 -
  that respond to initiating events to prevent undesirable consequences (i.e., core
  damage). Specifically, this issue relates to the availability and reliability examples of the
  equipment performance attribute because a latent common mode failure mechanism
  was not correctly evaluated. The inspectors evaluated the significance of this finding
  using Phase 1 of Inspection Manual Chapter 0609, Appendix A, "Significance
Enclosure 2
  Determination of Reactor Inspection Findings for At Power Situations," and determined
determined that this finding was more than minor because it is associated with the  
  that the finding was of very low safety significance (Green) because the issue was not a
equipment performance attribute for the Mitigating Systems Cornerstone, and it affected  
  design or qualification deficiency confirmed to result in loss of operability or functionality,
the cornerstone objective to ensure the availability, reliability, and capability of systems  
  did not represent a loss of system safety function, an actual loss of safety function of a
that respond to initiating events to prevent undesirable consequences (i.e., core  
  single train for greater than its technical specification allowed outage time, an actual loss
damage). Specifically, this issue relates to the availability and reliability examples of the  
  of safety function of a nontechnical specification risk-significant equipment train, and did
equipment performance attribute because a latent common mode failure mechanism  
  not screen as potentially risk significant due to a seismic, flooding, or severe weather
was not correctly evaluated. The inspectors evaluated the significance of this finding  
  initiating event. The cause of the finding has a problem identification and resolution
using Phase 1 of Inspection Manual Chapter 0609, Appendix A, "Significance  
  crosscutting aspect in the area associated with the corrective action program because
Determination of Reactor Inspection Findings for At Power Situations," and determined  
  Wolf Creek failed to thoroughly evaluate the failure mechanism such that the resolutions
that the finding was of very low safety significance (Green) because the issue was not a  
  address the causes and extent of conditions, as necessary [P.1.c].
design or qualification deficiency confirmed to result in loss of operability or functionality,  
  Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,
did not represent a loss of system safety function, an actual loss of safety function of a  
  and Drawings, requires, in part, that activities affecting quality shall be prescribed by
single train for greater than its technical specification allowed outage time, an actual loss  
  documented instructions or procedures of a type appropriate to the circumstances,
of safety function of a nontechnical specification risk-significant equipment train, and did  
  accomplished in accordance with those instructions or procedures, and contain
not screen as potentially risk significant due to a seismic, flooding, or severe weather  
  acceptance criteria to demonstrate that the activity was successfully accomplished.
initiating event. The cause of the finding has a problem identification and resolution  
  Procedure AP 26C-004, Technical Specification Operability, Revision 20, implements
crosscutting aspect in the area associated with the corrective action program because  
  this requirement and states, in part, that continued operability decisions shall be made in
Wolf Creek failed to thoroughly evaluate the failure mechanism such that the resolutions  
  accordance with Procedure AP 28-001, Operability Evaluations, Revision 17.
address the causes and extent of conditions, as necessary [P.1.c].  
  Procedure AP 28-001 requires, in part, that operability evaluations shall demonstrate
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,  
  that equipment meets its design functions. Per Sections 3.9(B) and 9.2.1 of the USAR,
and Drawings, requires, in part, that activities affecting quality shall be prescribed by  
  the essential service water pumps are designed to withstand a safe shutdown
documented instructions or procedures of a type appropriate to the circumstances,  
  earthquake. Contrary to the above, from November 1, 2009, to January 13, 2010,
accomplished in accordance with those instructions or procedures, and contain  
  Operability Evaluation EF-09-010, Revisions 0 and 1, did not demonstrate that the
acceptance criteria to demonstrate that the activity was successfully accomplished.
  essential service water pumps could withstand a safe shutdown earthquake.
Procedure AP 26C-004, Technical Specification Operability, Revision 20, implements  
  Specifically, no calculations existed to demonstrate allowable stresses and pump
this requirement and states, in part, that continued operability decisions shall be made in  
  impeller clearances. Because the finding is of very low safety significance and has been
accordance with Procedure AP 28-001, Operability Evaluations, Revision 17.
  entered into the corrective action program as Condition Reports 22798 and 21572, this
Procedure AP 28-001 requires, in part, that operability evaluations shall demonstrate  
  violation is being treated as a noncited violation, consistent with Section VI.A of the
that equipment meets its design functions. Per Sections 3.9(B) and 9.2.1 of the USAR,  
  NRC Enforcement Policy: NCV 05000482/2009005-08, Inadequate Operability
the essential service water pumps are designed to withstand a safe shutdown  
  Evaluation of Essential Service Water Pumps.
earthquake. Contrary to the above, from November 1, 2009, to January 13, 2010,  
.2 Introduction. The inspectors identified a Green, noncited violation of Technical
Operability Evaluation EF-09-010, Revisions 0 and 1, did not demonstrate that the  
  Specification 3.3.1, Condition I, for making positive reactivity addition prohibited by
essential service water pumps could withstand a safe shutdown earthquake.
  technical specifications in Mode 2 because one source range nuclear instrument
Specifically, no calculations existed to demonstrate allowable stresses and pump  
  channel was inoperable.
impeller clearances. Because the finding is of very low safety significance and has been  
  Description. On August 19, 2009, at 3:47 p.m., a loss of offsite power and reactor trip
entered into the corrective action program as Condition Reports 22798 and 21572, this  
  occurred. As a result, cavity cooling fans were lost causing an increase in air
violation is being treated as a noncited violation, consistent with Section VI.A of the  
                                        - 41 -                                    Enclosure 2
NRC Enforcement Policy: NCV 05000482/2009005-08, Inadequate Operability  
Evaluation of Essential Service Water Pumps.  
.2  
Introduction. The inspectors identified a Green, noncited violation of Technical  
Specification 3.3.1, Condition I, for making positive reactivity addition prohibited by  
technical specifications in Mode 2 because one source range nuclear instrument  
channel was inoperable.  
Description. On August 19, 2009, at 3:47 p.m., a loss of offsite power and reactor trip  
occurred. As a result, cavity cooling fans were lost causing an increase in air  


temperature in the reactor cavity. Shortly thereafter, the indicated count rate on source
range nuclear instrument NI-31 began increasing from the expected value of about 250
counts per minute (cpm) to 15,000 cpm and then to a maximum of 27,000 cpm over an
- 42 -
8-hour period. Control room operators declared the source range channel NI-31
inoperable as a result of this abnormal behavior. Power to the cavity fans was restored
around 1 a.m. on August 20, 2009, and the source range nuclear instrument NI-31 count
rate returned to its expected value below 250 cpm, based on its anticipated reading
relative to source range NI-32 which did not experience any increase in count rate with a
Enclosure 2
loss of cavity cooling.
temperature in the reactor cavity. Shortly thereafter, the indicated count rate on source  
Wolf Creek concluded, based on feedback from the vendor, the most likely cause of the
range nuclear instrument NI-31 began increasing from the expected value of about 250  
abnormal readings was moisture intrusion at the cable to detector connection at the
counts per minute (cpm) to 15,000 cpm and then to a maximum of 27,000 cpm over an  
base of the detector inside the reactor cavity. As long as cavity cooling remained
8-hour period. Control room operators declared the source range channel NI-31  
available, the moisture intrusion would not be an issue. Based on this information, Wolf
inoperable as a result of this abnormal behavior. Power to the cavity fans was restored  
Creek declared the source range NI-31 operable restarted from the forced outage on
around 1 a.m. on August 20, 2009, and the source range nuclear instrument NI-31 count  
August 23, 2009. Wolf Creeks operability evaluation failed to identify that safety-related
rate returned to its expected value below 250 cpm, based on its anticipated reading  
equipment was now reliant on nonsafety cavity cooling fans and nonsafety electrical
relative to source range NI-32 which did not experience any increase in count rate with a  
power to those fans. The source range instruments NI-31 and -32 are required to be
loss of cavity cooling.  
operable in Mode 2 below the P-6 interlock to monitor the approach to criticality.
Wolf Creek concluded, based on feedback from the vendor, the most likely cause of the  
During this time, the resident inspectors questioned the operability of source range
abnormal readings was moisture intrusion at the cable to detector connection at the  
instrument NI-31. When entering Refueling Outage 17, a power supply failure in the
base of the detector inside the reactor cavity. As long as cavity cooling remained  
control cabinet caused source range NI-31 to fail upon demand during shutdown. On
available, the moisture intrusion would not be an issue. Based on this information, Wolf  
October 7, 2009, Wolf Creek performed another operability evaluation that stated that
Creek declared the source range NI-31 operable restarted from the forced outage on  
the source range was operable because it had passed its surveillance tests during the
August 23, 2009. Wolf Creeks operability evaluation failed to identify that safety-related  
last refueling outage that ended in May 2008. The inspectors noted that this evaluation
equipment was now reliant on nonsafety cavity cooling fans and nonsafety electrical  
did not address the observed problem and therefore did not provide a reasonable basis
power to those fans. The source range instruments NI-31 and -32 are required to be  
for operability. On October 28, 2009, during interviews with Wolf Creek engineering
operable in Mode 2 below the P-6 interlock to monitor the approach to criticality.  
personnel, the inspectors learned that the original operability determination used to
During this time, the resident inspectors questioned the operability of source range  
restart from the forced outage was inaccurate because the equipment configuration in
instrument NI-31. When entering Refueling Outage 17, a power supply failure in the  
the field was different than described in the operability determination. The detectors are
control cabinet caused source range NI-31 to fail upon demand during shutdown. On  
in fact hard wired and there are no cabling connections until the containment bio-shield
October 7, 2009, Wolf Creek performed another operability evaluation that stated that  
wall, therefore, no connectors would be affected by the reactor cavity temperature
the source range was operable because it had passed its surveillance tests during the  
increase following the loss of cavity cooling fans. Consequently, there was no valid
last refueling outage that ended in May 2008. The inspectors noted that this evaluation  
explanation for the increase in count rate observed on August 19, 2009. Shortly
did not address the observed problem and therefore did not provide a reasonable basis  
thereafter, Wolf Creek replaced the source range NI-31 detector before restart from
for operability. On October 28, 2009, during interviews with Wolf Creek engineering  
Refueling Outage 17 to definitively restore operability to the channel.
personnel, the inspectors learned that the original operability determination used to  
On November 13, 2009, the resident inspectors observed the removal of source range
restart from the forced outage was inaccurate because the equipment configuration in  
Detector SE-0031 from the reactor cavity. There was some minor damage to the outer
the field was different than described in the operability determination. The detectors are  
layer of cable wrap, however, nothing was observed that could conclusively explain the
in fact hard wired and there are no cabling connections until the containment bio-shield  
detectors malfunction on August 19, 2009, or ensure its future operability. Wolf Creek
wall, therefore, no connectors would be affected by the reactor cavity temperature  
USAR, Chapter 15, credits low power reactor trips as being terminated by the power
increase following the loss of cavity cooling fans. Consequently, there was no valid  
range instruments. The power range instruments are not required to be operable in
explanation for the increase in count rate observed on August 19, 2009. Shortly  
Mode 3. USAR, Chapter 15, credits the source range and intermediate range reactor
thereafter, Wolf Creek replaced the source range NI-31 detector before restart from  
trips to stop reactivity excursions at a much lower power. This allows technical
Refueling Outage 17 to definitively restore operability to the channel.  
specifications to credit these trips in Mode 3. During the shutdown in August 2009, rod
On November 13, 2009, the resident inspectors observed the removal of source range  
drive motor-generator set testing was performed which cycled the reactor trip breakers
Detector SE-0031 from the reactor cavity. There was some minor damage to the outer  
                                      - 42 -                                Enclosure 2
layer of cable wrap, however, nothing was observed that could conclusively explain the  
detectors malfunction on August 19, 2009, or ensure its future operability. Wolf Creek  
USAR, Chapter 15, credits low power reactor trips as being terminated by the power  
range instruments. The power range instruments are not required to be operable in  
Mode 3. USAR, Chapter 15, credits the source range and intermediate range reactor  
trips to stop reactivity excursions at a much lower power. This allows technical  
specifications to credit these trips in Mode 3. During the shutdown in August 2009, rod  
drive motor-generator set testing was performed which cycled the reactor trip breakers  


    and made the control rods capable of withdrawal. The inspectors also reviewed the
    technical specification bases for the source range which stated that they are required to
    perform a monitoring function of neutron levels and provide indication of reactivity
- 43 -
    changes that may occur.
    Analysis. Reactivity addition with source range channel nuclear instrument-31
    inoperable is a performance deficiency. The finding was more than minor because it
    was associated with the configuration control (reactivity control) attribute of the Barrier
    Integrity Cornerstone, and it affected the cornerstone objective to provide reasonable
Enclosure 2
    assurance that physical design barriers (fuel cladding, reactor coolant system, and
and made the control rods capable of withdrawal. The inspectors also reviewed the  
    containment) protect the public from radionuclide releases caused by accidents or
technical specification bases for the source range which stated that they are required to  
    events. The inspectors evaluated the significance of this finding using Phase 1 of
perform a monitoring function of neutron levels and provide indication of reactivity  
    Inspection Manual Chapter 0609.04, and determined that the finding screened to Green
changes that may occur.  
    because the finding only affected the fuel barrier. Additionally, the cause of the finding
Analysis. Reactivity addition with source range channel nuclear instrument-31  
    has a human performance crosscutting aspect in the area associated with the decision
inoperable is a performance deficiency. The finding was more than minor because it  
    making. Specifically, Wolf Creek did not use conservative assumptions in decision
was associated with the configuration control (reactivity control) attribute of the Barrier  
    making and adopt requirements to demonstrate that the proposed action is safe in order
Integrity Cornerstone, and it affected the cornerstone objective to provide reasonable  
    to proceed rather than a requirement to demonstrate that it is unsafe in order to
assurance that physical design barriers (fuel cladding, reactor coolant system, and  
    disapprove the action, when performing an operability evaluation for the source range
containment) protect the public from radionuclide releases caused by accidents or  
    Nuclear Instrument 31 detector prior to restarting from a forced outage [H.1(b)].
events. The inspectors evaluated the significance of this finding using Phase 1 of  
    Enforcement. Wolf Creek Technical Specification LCO 3.3.1 Reactor Trip System
Inspection Manual Chapter 0609.04, and determined that the finding screened to Green  
    Instrumentation, Condition I, requires immediate suspension of all operations activities
because the finding only affected the fuel barrier. Additionally, the cause of the finding  
    involving positive reactivity additions when one source range channel is inoperable while
has a human performance crosscutting aspect in the area associated with the decision  
    in Mode 2. Contrary to the above on August 22, 2009, at 11:10 a.m., Wolf Creek
making. Specifically, Wolf Creek did not use conservative assumptions in decision  
    entered Mode 2 with one source range channel inoperable and continued withdrawing
making and adopt requirements to demonstrate that the proposed action is safe in order  
    control rods until the reactor was critical at 11:54 a.m. At that time, Wolf Creek went
to proceed rather than a requirement to demonstrate that it is unsafe in order to  
    above the P-6 interlock and source range monitoring was no longer required by technical
disapprove the action, when performing an operability evaluation for the source range  
    specifications. Because the finding is of very low safety significance and has been
Nuclear Instrument 31 detector prior to restarting from a forced outage [H.1(b)].  
    entered into the corrective action program as Condition Report 20208, this violation is
Enforcement. Wolf Creek Technical Specification LCO 3.3.1 Reactor Trip System  
    being treated as a noncited violation, consistent with Section VI.A of the NRC
Instrumentation, Condition I, requires immediate suspension of all operations activities  
    Enforcement Policy: NCV 05000482/2009005-09, Positive Reactivity Addition
involving positive reactivity additions when one source range channel is inoperable while  
    Prohibited by technical specifications while in Mode 2.
in Mode 2. Contrary to the above on August 22, 2009, at 11:10 a.m., Wolf Creek  
1R18 Plant Modifications (71111.18)
entered Mode 2 with one source range channel inoperable and continued withdrawing  
    Permanent Modifications
control rods until the reactor was critical at 11:54 a.m. At that time, Wolf Creek went  
    The inspectors reviewed key affected parameters associated with energy needs,
above the P-6 interlock and source range monitoring was no longer required by technical  
    materials, replacement components, timing, heat removal, control signals, equipment
specifications. Because the finding is of very low safety significance and has been  
    protection from hazards, operations, flow paths, pressure boundary, ventilation
entered into the corrective action program as Condition Report 20208, this violation is  
    boundary, structural, process medium properties, licensing basis, and failure modes for
being treated as a noncited violation, consistent with Section VI.A of the NRC  
    the permanent modifications listed below.
Enforcement Policy: NCV 05000482/2009005-09, Positive Reactivity Addition  
    *       December 16, 2009, Instrument setpoints for reactor coolant pump thermal
Prohibited by technical specifications while in Mode 2.  
            barrier isolation and Valve EGHV62
                                          - 43 -                                  Enclosure 2
1R18 Plant Modifications (71111.18)  
Permanent Modifications  
The inspectors reviewed key affected parameters associated with energy needs,  
materials, replacement components, timing, heat removal, control signals, equipment  
protection from hazards, operations, flow paths, pressure boundary, ventilation  
boundary, structural, process medium properties, licensing basis, and failure modes for  
the permanent modifications listed below.  
*  
December 16, 2009, Instrument setpoints for reactor coolant pump thermal  
barrier isolation and Valve EGHV62


  The inspectors reviewed key parameters associated with energy needs, materials,
  replacement components, timing, heat removal, control signals, equipment protection
  from hazards, operations, flow paths, pressure boundary, ventilation boundary,
- 44 -
  structural, process medium properties, licensing basis, and failure modes for the
  permanent modification identified as configuration Change Package 013096.
  The inspectors verified that modification preparation, staging, and implementation did not
  impair emergency/abnormal operating procedure actions, key safety functions, or
  operator response to loss of key safety functions; postmodification testing will maintain
Enclosure 2
  the plant in a safe configuration during testing by verifying that unintended system
The inspectors reviewed key parameters associated with energy needs, materials,  
  interactions will not occur; systems, structures and components, performance
replacement components, timing, heat removal, control signals, equipment protection  
  characteristics still meet the design basis; the modification design assumptions were
from hazards, operations, flow paths, pressure boundary, ventilation boundary,  
  appropriate; the modification test acceptance criteria will be met; and licensee personnel
structural, process medium properties, licensing basis, and failure modes for the  
  identified and implemented appropriate corrective actions associated with permanent
permanent modification identified as configuration Change Package 013096.  
  plant modifications. Specific documents reviewed during this inspection are listed in the
  attachment.
The inspectors verified that modification preparation, staging, and implementation did not  
  These activities constitute completion of one sample for permanent plant modifications
impair emergency/abnormal operating procedure actions, key safety functions, or  
  as defined in Inspection Procedure IP 71111.18-05.
operator response to loss of key safety functions; postmodification testing will maintain  
b. Findings
the plant in a safe configuration during testing by verifying that unintended system  
  Introduction. On December 16, 2009, inspectors identified a Green noncited violation of
interactions will not occur; systems, structures and components, performance  
  10 CFR Part 50, Appendix B, Criterion III, Design Control, involving failure to obtain
characteristics still meet the design basis; the modification design assumptions were  
  vendor design data for a modification.
appropriate; the modification test acceptance criteria will be met; and licensee personnel  
  Description. On December 16, 2009, the inspectors reviewed configuration change
identified and implemented appropriate corrective actions associated with permanent  
  Package 013096 from August 2009 which modified the upper flow limit through the
plant modifications. Specific documents reviewed during this inspection are listed in the  
  reactor coolant pump thermal barrier heat exchangers from 60 to 68 gpm. The change
attachment.  
  package cited an internal memo from 1992 as the justification for the increased flow.
  The inspectors reviewed the internal memo and noted that it described the thermal
These activities constitute completion of one sample for permanent plant modifications  
  barrier outlet valves going closed on high flow. It also indirectly described a telephone
as defined in Inspection Procedure IP 71111.18-05.  
  conversation with a Westinghouse representative who stated that the thermal barriers
  were capable of up to 90 gpm sustained flow. The inspectors found no accompanying
b.  
  data from Westinghouse to justify this claim. Procedure AP 05-005, Design Control,
Findings  
  required that vendor data be obtained in accordance with Procedure AP 05-013, Review
Introduction. On December 16, 2009, inspectors identified a Green noncited violation of  
  of Vendor Technical Documents, Revision 7A. The inspectors reviewed
10 CFR Part 50, Appendix B, Criterion III, Design Control, involving failure to obtain  
  Procedure AP 05-013 and noted that it stated that documentation would be obtained
vendor design data for a modification.  
  from the vendor consistent with procurement standards for acceptance.
Description. On December 16, 2009, the inspectors reviewed configuration change  
  Procedure AP 05-013, step 6.5, specified evaluation of vendor technical documentation,
Package 013096 from August 2009 which modified the upper flow limit through the  
  but it did not specify how to disposition informal information. This step required a review
reactor coolant pump thermal barrier heat exchangers from 60 to 68 gpm. The change  
  of vendor documentation by engineering to ensure design requirements are met.
package cited an internal memo from 1992 as the justification for the increased flow.
  Procedure AP 05-013, step 6.6, specified incorporating changes to vendor documents
The inspectors reviewed the internal memo and noted that it described the thermal  
  that originate with Wolf Creek, but it did not specify that the vendor must be contacted for
barrier outlet valves going closed on high flow. It also indirectly described a telephone  
  changes that Wolf Creek has not evaluated.
conversation with a Westinghouse representative who stated that the thermal barriers  
  Procedure AP 05-002, Dispositions and Change Packages, Revision 8, specified how
were capable of up to 90 gpm sustained flow. The inspectors found no accompanying  
  Wolf Creek prepares, documents, and implements modifications to plant equipment and
data from Westinghouse to justify this claim. Procedure AP 05-005, Design Control,  
                                      - 44 -                                    Enclosure 2
required that vendor data be obtained in accordance with Procedure AP 05-013, Review  
of Vendor Technical Documents, Revision 7A. The inspectors reviewed  
Procedure AP 05-013 and noted that it stated that documentation would be obtained  
from the vendor consistent with procurement standards for acceptance.
Procedure AP 05-013, step 6.5, specified evaluation of vendor technical documentation,  
but it did not specify how to disposition informal information. This step required a review  
of vendor documentation by engineering to ensure design requirements are met.
Procedure AP 05-013, step 6.6, specified incorporating changes to vendor documents  
that originate with Wolf Creek, but it did not specify that the vendor must be contacted for  
changes that Wolf Creek has not evaluated.  
Procedure AP 05-002, Dispositions and Change Packages, Revision 8, specified how  
Wolf Creek prepares, documents, and implements modifications to plant equipment and  


design documents. Procedure AP 05-002, step 6.4.5, required that the data be obtained
from the vendor and placed in the modification package supporting the plant change.
Procedure AP 05-002, step 6.4.6.6, did not allow informal communications to form the
- 45 -
basis for a modification. Telephone calls are defined as informal communication per
Procedure AP 05-005. The inspectors found no documentation to show validation of the
verbal data provided by the vendor. This modification was a corrective action to
VIO 05000482/2009002-07 (EA-09-110). This notice of violation will remain open until
full compliance has been restored. Wolf Creek subsequently consulted with
Enclosure 2
Westinghouse to confirm the acceptability of the increased flow rate, and requested a
design documents. Procedure AP 05-002, step 6.4.5, required that the data be obtained  
formal calculation. This issue is captured in Condition Report 22824.
from the vendor and placed in the modification package supporting the plant change.
Analysis. The inspectors found that the failure to follow procedure for the modification
Procedure AP 05-002, step 6.4.6.6, did not allow informal communications to form the  
was a performance deficiency. Traditional enforcement does not apply since there were
basis for a modification. Telephone calls are defined as informal communication per  
no actual safety consequences or potential for impacting the NRC's regulatory function,
Procedure AP 05-005. The inspectors found no documentation to show validation of the  
and the finding was not the result of any willful violation of NRC requirements or Wolf
verbal data provided by the vendor. This modification was a corrective action to  
Creek procedures. The inspectors determined that this finding was more than minor
VIO 05000482/2009002-07 (EA-09-110). This notice of violation will remain open until  
because this issue aligned with Inspection Manual Chapter 0612, Appendix E,
full compliance has been restored. Wolf Creek subsequently consulted with  
example 2.f, in that the modification relied on verbal statements to raise the allowable
Westinghouse to confirm the acceptability of the increased flow rate, and requested a  
flow through the heat exchanger. This is a significant deficiency in the modification
formal calculation. This issue is captured in Condition Report 22824.  
package. The inspectors determined this finding was associated with the design control
Analysis. The inspectors found that the failure to follow procedure for the modification  
attribute of the Initiating Events Cornerstone and affected the cornerstone objective to
was a performance deficiency. Traditional enforcement does not apply since there were  
limit the likelihood of events that upset plant stability and challenge critical safety
no actual safety consequences or potential for impacting the NRC's regulatory function,  
functions. The inspectors evaluated the significance of this finding using Phase 1 of
and the finding was not the result of any willful violation of NRC requirements or Wolf  
Inspection Manual Chapter 0609.04 and determined that the finding was of very low
Creek procedures. The inspectors determined that this finding was more than minor  
safety significance because assuming worst case degradation, the finding would not
because this issue aligned with Inspection Manual Chapter 0612, Appendix E,  
result in exceeding the technical specification limit for identified reactor coolant system
example 2.f, in that the modification relied on verbal statements to raise the allowable  
leakage and would not have likely affected other mitigation systems resulting in a total
flow through the heat exchanger. This is a significant deficiency in the modification  
loss of their safety function because seal injection was available. This finding has a
package. The inspectors determined this finding was associated with the design control  
crosscutting aspect in the area of human performance associated with work practices in
attribute of the Initiating Events Cornerstone and affected the cornerstone objective to  
that management was unsuccessful in communicating expectations on procedure use
limit the likelihood of events that upset plant stability and challenge critical safety  
and adherence in engineering [H.4.b].
functions. The inspectors evaluated the significance of this finding using Phase 1 of  
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control," requires,
Inspection Manual Chapter 0609.04 and determined that the finding was of very low  
in part, that the licensee establish measures for the identification and control of design
safety significance because assuming worst case degradation, the finding would not  
interfaces and for coordination among participating design organizations. These
result in exceeding the technical specification limit for identified reactor coolant system  
measures shall include the establishment of procedures among participating design
leakage and would not have likely affected other mitigation systems resulting in a total  
organizations for the review, approval, release, distribution, and revision of documents
loss of their safety function because seal injection was available. This finding has a  
involving design interfaces. It also requires, in part, that design changes shall be subject
crosscutting aspect in the area of human performance associated with work practices in  
to design control measures commensurate with those applied to the original design.
that management was unsuccessful in communicating expectations on procedure use  
Procedures AP 05-005 and AP 05-002 implement this requirement by requiring formal
and adherence in engineering [H.4.b].  
vendor data required for modifications to be incorporated into modifications. Contrary to
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control," requires,  
the above, from August 13, 2009, to December 31, 2009, Wolf Creek failed to obtain
in part, that the licensee establish measures for the identification and control of design  
vendor design data for configuration change Package 013096 in accordance with
interfaces and for coordination among participating design organizations. These  
Procedures AP 05-005 and AP 05-002. Because the finding is of very low safety
measures shall include the establishment of procedures among participating design  
significance and has been entered into the corrective action program as Condition
organizations for the review, approval, release, distribution, and revision of documents  
Report 22824, this violation is being treated as a noncited violation, consistent with
involving design interfaces. It also requires, in part, that design changes shall be subject  
Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-10, Failure to
to design control measures commensurate with those applied to the original design.
Obtain Vendor Data Necessary for Plant Modification.
Procedures AP 05-005 and AP 05-002 implement this requirement by requiring formal  
                                    - 45 -                                      Enclosure 2
vendor data required for modifications to be incorporated into modifications. Contrary to  
the above, from August 13, 2009, to December 31, 2009, Wolf Creek failed to obtain  
vendor design data for configuration change Package 013096 in accordance with  
Procedures AP 05-005 and AP 05-002. Because the finding is of very low safety  
significance and has been entered into the corrective action program as Condition  
Report 22824, this violation is being treated as a noncited violation, consistent with  
Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-10, Failure to  
Obtain Vendor Data Necessary for Plant Modification.  


1R19 Postmaintenance Testing (71111.19)
  a. Inspection Scope
    The inspectors reviewed the following postmaintenance activities to verify that
- 46 -
    procedures and test activities were adequate to ensure system operability and functional
    capability:
      *     October 23, 2009, Emergency diesel generator A run after replacement of speed
            switch
    *       October 23, 2009, Instrumentation and control testing of emergency diesel
Enclosure 2
            generator A instrument power supply
1R19 Postmaintenance Testing (71111.19)
    *       November 6, 2009, Essential service water train B pump and motor replacement
a.  
    *       November 2, 2009, Motor-operated valve MOV 8811A after actuator and internals
Inspection Scope  
            replacement
The inspectors reviewed the following postmaintenance activities to verify that  
    The inspectors selected these activities based upon the structure, system, or
procedures and test activities were adequate to ensure system operability and functional  
    component's ability to affect risk. The inspectors evaluated these activities for the
capability:  
    following (as applicable):
*  
    *       The effect of testing on the plant had been adequately addressed; testing was
October 23, 2009, Emergency diesel generator A run after replacement of speed  
            adequate for the maintenance performed
switch  
    *       Acceptance criteria were clear and demonstrated operational readiness; test
*  
            instrumentation was appropriate
October 23, 2009, Instrumentation and control testing of emergency diesel  
    The inspectors evaluated the activities against the technical specifications, the USAR,
generator A instrument power supply  
    10 CFR Part 50 requirements, licensee procedures, and various NRC generic
*  
    communications to ensure that the test results adequately ensured that the equipment
November 6, 2009, Essential service water train B pump and motor replacement
    met the licensing basis and design requirements. In addition, the inspectors reviewed
*  
    corrective action documents associated with postmaintenance tests to determine
November 2, 2009, Motor-operated valve MOV 8811A after actuator and internals  
    whether the licensee was identifying problems and entering them in the corrective action
replacement  
    program and that the problems were being corrected commensurate with their
The inspectors selected these activities based upon the structure, system, or  
    importance to safety. Specific documents reviewed during this inspection are listed in
component's ability to affect risk. The inspectors evaluated these activities for the  
    the attachment.
following (as applicable):  
    These activities constitute completion of four postmaintenance testing inspection
*  
    samples as defined in Inspection Procedure IP 71111.19-05.
The effect of testing on the plant had been adequately addressed; testing was  
  b. Findings
adequate for the maintenance performed  
    No findings of significance were identified.
*  
                                        - 46 -                                  Enclosure 2
Acceptance criteria were clear and demonstrated operational readiness; test  
instrumentation was appropriate  
The inspectors evaluated the activities against the technical specifications, the USAR,  
10 CFR Part 50 requirements, licensee procedures, and various NRC generic  
communications to ensure that the test results adequately ensured that the equipment  
met the licensing basis and design requirements. In addition, the inspectors reviewed  
corrective action documents associated with postmaintenance tests to determine  
whether the licensee was identifying problems and entering them in the corrective action  
program and that the problems were being corrected commensurate with their  
importance to safety. Specific documents reviewed during this inspection are listed in  
the attachment.  
These activities constitute completion of four postmaintenance testing inspection  
samples as defined in Inspection Procedure IP 71111.19-05.  
b.  
Findings  
No findings of significance were identified.  


1R20 Refueling and Other Outage Activities (71111.20)
  a. Inspection Scope
    The inspectors reviewed the outage safety plan and contingency plans for the Wolf
- 47 -
    Creek refueling outage, conducted from October 10 to November 17 2009, to confirm
    that licensee personnel had appropriately considered risk, industry experience, and
    previous site-specific problems in developing and implementing a plan that assured
    maintenance of defense in depth. During the refueling outage, the inspectors observed
    portions of the shutdown and cooldown processes and monitored licensee controls over
Enclosure 2
    the outage activities listed below.
1R20 Refueling and Other Outage Activities (71111.20)
    *       Configuration management, including maintenance of defense in depth, is
a.  
              commensurate with the outage safety plan for key safety functions and
Inspection Scope  
              compliance with the applicable technical specifications when taking equipment
The inspectors reviewed the outage safety plan and contingency plans for the Wolf  
              out of service.
Creek refueling outage, conducted from October 10 to November 17 2009, to confirm  
    *       Clearance activities, including confirmation that tags were properly hung and
that licensee personnel had appropriately considered risk, industry experience, and  
              equipment appropriately configured to safely support the work or testing.
previous site-specific problems in developing and implementing a plan that assured  
    *       Installation and configuration of reactor coolant pressure, level, and temperature
maintenance of defense in depth. During the refueling outage, the inspectors observed  
              instruments to provide accurate indication, accounting for instrument error.
portions of the shutdown and cooldown processes and monitored licensee controls over  
    *       Status and configuration of electrical systems to ensure that technical
the outage activities listed below.  
              specifications and outage safety-plan requirements were met, and controls over
*  
              switchyard activities.
Configuration management, including maintenance of defense in depth, is  
    *       Monitoring of decay heat removal processes, systems, and components.
commensurate with the outage safety plan for key safety functions and  
    *       Verification that outage work was not impacting the ability of the operators to
compliance with the applicable technical specifications when taking equipment  
              operate the spent fuel pool cooling system.
out of service.  
    *       Reactor water inventory controls, including flow paths, configurations, and
*  
              alternative means for inventory addition, and controls to prevent inventory loss.
Clearance activities, including confirmation that tags were properly hung and  
    *       Controls over activities that could affect reactivity.
equipment appropriately configured to safely support the work or testing.  
    *       Maintenance of secondary containment as required by the technical
*  
              specifications.
Installation and configuration of reactor coolant pressure, level, and temperature  
    *       Refueling activities, including fuel handling and sipping to detect fuel assembly
instruments to provide accurate indication, accounting for instrument error.  
              leakage.
*  
    *       Startup and ascension to full power operation, tracking of startup prerequisites,
Status and configuration of electrical systems to ensure that technical  
              walkdown of the drywell (primary containment) to verify that debris had not been
specifications and outage safety-plan requirements were met, and controls over  
              left which could block emergency core cooling system suction strainers, and
switchyard activities.  
              reactor physics testing.
*  
                                          - 47 -                                  Enclosure 2
Monitoring of decay heat removal processes, systems, and components.  
*  
Verification that outage work was not impacting the ability of the operators to  
operate the spent fuel pool cooling system.  
*  
Reactor water inventory controls, including flow paths, configurations, and  
alternative means for inventory addition, and controls to prevent inventory loss.  
*  
Controls over activities that could affect reactivity.  
*  
Maintenance of secondary containment as required by the technical  
specifications.  
*  
Refueling activities, including fuel handling and sipping to detect fuel assembly  
leakage.  
*  
Startup and ascension to full power operation, tracking of startup prerequisites,  
walkdown of the drywell (primary containment) to verify that debris had not been  
left which could block emergency core cooling system suction strainers, and  
reactor physics testing.  


      *       Licensee identification and resolution of problems related to refueling outage
              activities.
      Specific documents reviewed during this inspection are listed in the attachment.
- 48 -
      These activities constitute completion of one refueling outage and other outage
      inspection sample as defined in Inspection Procedure IP 71111.20-05.
  b. Findings
.1   Introduction. The inspectors identified a Green cited violation of 10 CFR Part 50,
      Appendix B, Criterion III, Design Control, for failure to correct a previous violation for an
Enclosure 2
      inadequate vent path for the reactor vessel head.
*  
      Description. NRC Inspection Report 05000482/2008004 documented a Green noncited
Licensee identification and resolution of problems related to refueling outage  
      violation of 10 CFR Part 50, Criterion III, Design Control, associated with the formation
activities.  
      of voids in the reactor vessel head during refueling outages.
Specific documents reviewed during this inspection are listed in the attachment.  
      During Refueling Outage 17 on October 13, 2009, Wolf Creek depressurized the reactor
These activities constitute completion of one refueling outage and other outage  
      and drained the reactor coolant system via the pressurizer to a level 374 inches above
inspection sample as defined in Inspection Procedure IP 71111.20-05.  
      the bottom of the hot leg. Reactor coolant system pressure was established at
b.  
      atmospheric pressure, approximately 6-10 psig below the volume control tank pressure.
Findings  
      These actions were performed in accordance with plant operating
.1  
      Procedure SYS BB-215, RCS Drain Down with Fuel in Reactor. The operators
Introduction. The inspectors identified a Green cited violation of 10 CFR Part 50,  
      completed Sections 6.1 and 6.2 of the procedure to vent the reactor vessel head to the
Appendix B, Criterion III, Design Control, for failure to correct a previous violation for an  
      pressurizer and purge the pressurizer with nitrogen.
inadequate vent path for the reactor vessel head.  
      Control room operators subsequently initiated Condition Reports 20648 and 20633 to
Description. NRC Inspection Report 05000482/2008004 documented a Green noncited  
      identify anomalous readings in pressurizer and reactor vessel level. The inspectors
violation of 10 CFR Part 50, Criterion III, Design Control, associated with the formation  
      reviewed plant computer data from October 11 to 14, 2009, and confirmed that a void
of voids in the reactor vessel head during refueling outages.  
      had formed in the reactor vessel head region following reactor coolant system
During Refueling Outage 17 on October 13, 2009, Wolf Creek depressurized the reactor  
      depressurization. As the gas built up, it forced primary coolant out of the reactor vessel
and drained the reactor coolant system via the pressurizer to a level 374 inches above  
      and into the pressurizer over many hours, causing the observed level changes.
the bottom of the hot leg. Reactor coolant system pressure was established at  
      Following the previous refueling outage, Wolf Creek Mode 5 Procedure GEN 00-009 had
atmospheric pressure, approximately 6-10 psig below the volume control tank pressure.
      been changed to require reactor vessel level instrumentation system to be in service so
These actions were performed in accordance with plant operating  
      that control room operators could observe any decrease in reactor vessel level. Based
Procedure SYS BB-215, RCS Drain Down with Fuel in Reactor. The operators  
      on plant computer data, the observed change of approximately 41 inches in pressurizer
completed Sections 6.1 and 6.2 of the procedure to vent the reactor vessel head to the  
      level equated to a maximum void size of 1100 gallons of primary coolant in the reactor
pressurizer and purge the pressurizer with nitrogen.  
      vessel. Excluding the void, time to boil in the reactor coolant system was calculated to
Control room operators subsequently initiated Condition Reports 20648 and 20633 to  
      be 2.5 hours during outage planning.
identify anomalous readings in pressurizer and reactor vessel level. The inspectors  
      Following the formation of a similar void in Refueling Outage 16, Wolf Creek initiated a
reviewed plant computer data from October 11 to 14, 2009, and confirmed that a void  
      root cause evaluation during under Condition Report 2008-001032. The void size during
had formed in the reactor vessel head region following reactor coolant system  
      Refueling Outage 16 was 2600 gallons. Wolf Creek determined that the root cause was
depressurization. As the gas built up, it forced primary coolant out of the reactor vessel  
      a loop seal or blockage in the piping. The root cause described boron precipitation as a
and into the pressurizer over many hours, causing the observed level changes.
      possible source of the blockage. Corrective actions were subsequently planned for
Following the previous refueling outage, Wolf Creek Mode 5 Procedure GEN 00-009 had  
      Refueling Outage 17. The slope of the vessel head piping was verified to be correct to
been changed to require reactor vessel level instrumentation system to be in service so  
      ensure no loop seals was performed as a corrective action to prevent recurrence.
that control room operators could observe any decrease in reactor vessel level. Based  
                                          - 48 -                                    Enclosure 2
on plant computer data, the observed change of approximately 41 inches in pressurizer  
level equated to a maximum void size of 1100 gallons of primary coolant in the reactor  
vessel. Excluding the void, time to boil in the reactor coolant system was calculated to  
be 2.5 hours during outage planning.  
Following the formation of a similar void in Refueling Outage 16, Wolf Creek initiated a  
root cause evaluation during under Condition Report 2008-001032. The void size during  
Refueling Outage 16 was 2600 gallons. Wolf Creek determined that the root cause was  
a loop seal or blockage in the piping. The root cause described boron precipitation as a  
possible source of the blockage. Corrective actions were subsequently planned for  
Refueling Outage 17. The slope of the vessel head piping was verified to be correct to  
ensure no loop seals was performed as a corrective action to prevent recurrence.


However, after the piping slope was verified and loop seals ruled out as a possible
cause, no additional actions were taken to identify the cause of the inadequate vent. A
corrective action to perform an internal inspection of the vessel head was not performed
- 49 -
because Wolf Creek did not have tools to inspect around 90 bends in the piping. The
inspectors determined that Wolf Creek failed to identify the cause of the inadequate vent
path to relieve gases to the pressurizer, with the result that voiding would continue to be
a concern in the next refueling outage.
When the NRC issued NCV 05000482/2008004-07 on November 7, 2008, for the
Enclosure 2
reactor vessel head voiding during outages, corrective actions were tracked under
However, after the piping slope was verified and loop seals ruled out as a possible  
Condition Report 2008-001032. The inspectors concluded that Wolf Creek has yet to
cause, no additional actions were taken to identify the cause of the inadequate vent. A  
correct the inadequate vent path, allowing void formation to continue to occur in the
corrective action to perform an internal inspection of the vessel head was not performed  
reactor vessel head. Without an adequate vent from the top of the reactor vessel head
because Wolf Creek did not have tools to inspect around 90 bends in the piping. The  
to the pressurizer, noncondensable gas voids will form, decreasing reactor coolant
inspectors determined that Wolf Creek failed to identify the cause of the inadequate vent  
inventory and reducing the time to core boiling following a loss of shutdown cooling. The
path to relieve gases to the pressurizer, with the result that voiding would continue to be  
gas voids could grow to the top of the hot legs or until the driving head forces the void
a concern in the next refueling outage.  
past the blockage and into the gas space of the pressurizer, causing the plant to
When the NRC issued NCV 05000482/2008004-07 on November 7, 2008, for the  
inadvertently enter mid-loop operations. An adequate vent path is necessary to control
reactor vessel head voiding during outages, corrective actions were tracked under  
reactor coolant level. Wolf Creek has initiated a second root cause under Condition
Condition Report 2008-001032. The inspectors concluded that Wolf Creek has yet to  
Report 22501.
correct the inadequate vent path, allowing void formation to continue to occur in the  
Analysis. The inspectors determined that failure to provide an adequate vessel head
reactor vessel head. Without an adequate vent from the top of the reactor vessel head  
vent path to prevent gas accumulation in the reactor vessel during depressurized plant
to the pressurizer, noncondensable gas voids will form, decreasing reactor coolant  
operations was a performance deficiency. The inspectors determined that this finding
inventory and reducing the time to core boiling following a loss of shutdown cooling. The  
was associated with the design control attribute of the Initiating Events Cornerstone.
gas voids could grow to the top of the hot legs or until the driving head forces the void  
Specifically, the voiding reduces time to boil and impacted the cornerstone objective to
past the blockage and into the gas space of the pressurizer, causing the plant to  
limit the likelihood of those events that upset plant stability and challenge critical safety
inadvertently enter mid-loop operations. An adequate vent path is necessary to control  
functions during shutdown as well as power operations. The inspectors evaluated the
reactor coolant level. Wolf Creek has initiated a second root cause under Condition  
significance of this finding using Inspection Manual Chapter 0609, Appendix G,
Report 22501.  
Attachment 1, Shutdown Operations Significance Determination Process Phase 1
Analysis. The inspectors determined that failure to provide an adequate vessel head  
Operational Checklists for Both PWRs and BWRs. The inspectors determined that
vent path to prevent gas accumulation in the reactor vessel during depressurized plant  
Checklist 3 was applicable because the unit was in cold shutdown with the refueling
operations was a performance deficiency. The inspectors determined that this finding  
cavity level less than 23 feet. Based upon Appendix G, Attachment 1, Checklist 3,
was associated with the design control attribute of the Initiating Events Cornerstone.
Phase 2, analysis was not needed to characterize the risk significance of this finding
Specifically, the voiding reduces time to boil and impacted the cornerstone objective to  
because the level of loss was less than two feet, did not occur during reduced inventory,
limit the likelihood of those events that upset plant stability and challenge critical safety  
and appropriate action was taken regarding the level deviation. The finding was
functions during shutdown as well as power operations. The inspectors evaluated the  
determined to be of very low safety significance based upon the demonstrated
significance of this finding using Inspection Manual Chapter 0609, Appendix G,  
availability of mitigation systems and the reactor coolant system cavity inventory. The
Attachment 1, Shutdown Operations Significance Determination Process Phase 1  
inspectors determined the cause of the finding had a problem identification and
Operational Checklists for Both PWRs and BWRs. The inspectors determined that  
resolution aspect in the corrective action program. Specifically, Wolf Creeks corrective
Checklist 3 was applicable because the unit was in cold shutdown with the refueling  
actions were not successful to address the vent path blockage in a timely manner
cavity level less than 23 feet. Based upon Appendix G, Attachment 1, Checklist 3,  
[P.1(d)].
Phase 2, analysis was not needed to characterize the risk significance of this finding  
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,
because the level of loss was less than two feet, did not occur during reduced inventory,  
in part, that the design basis is correctly translated into specifications, drawings, and
and appropriate action was taken regarding the level deviation. The finding was  
procedures. The design basis of the reactor vessel head vent is to allow
determined to be of very low safety significance based upon the demonstrated  
noncondensable gases to escape to the pressurizer during shutdown conditions.
availability of mitigation systems and the reactor coolant system cavity inventory. The  
Contrary to the above, from December 2, 2003, to December 31, 2009, Wolf Creek
inspectors determined the cause of the finding had a problem identification and  
                                    - 49 -                                    Enclosure 2
resolution aspect in the corrective action program. Specifically, Wolf Creeks corrective  
actions were not successful to address the vent path blockage in a timely manner  
[P.1(d)].  
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,  
in part, that the design basis is correctly translated into specifications, drawings, and  
procedures. The design basis of the reactor vessel head vent is to allow  
noncondensable gases to escape to the pressurizer during shutdown conditions.
Contrary to the above, from December 2, 2003, to December 31, 2009, Wolf Creek  


  failed to ensure the design basis of the reactor vessel head vent was correctly translated
  into specifications, drawings, and procedures. Specifically, Wolf Creek designed and
  installed a reactor vessel head permanent vent piping modification which failed to vent
- 50 -
  noncondensable gases to the pressurizer during shutdown operations. This resulted in
  the formation of voids in the reactor vessel head while the plant was shutdown and
  depressurized in successive refueling outages. This issue and the corrective actions are
  being tracked by the licensee in Condition Reports 22501, 20648, 20568, and 20633.
  Due to the licensees failure to restore compliance from previous
Enclosure 2
  NCV 05000482/2008004-07 within a reasonable time after the violation was identified,
failed to ensure the design basis of the reactor vessel head vent was correctly translated  
  this violation is being cited as a Notice of Violation consistent with Section VI.A of the
into specifications, drawings, and procedures. Specifically, Wolf Creek designed and  
  Enforcement Policy: VIO 05000482/2009005-11, Failure to Correct Vessel Head Vent
installed a reactor vessel head permanent vent piping modification which failed to vent  
  Path (EA-10-020).
noncondensable gases to the pressurizer during shutdown operations. This resulted in  
.2 Introduction. The inspectors identified a Green noncited violation of Technical
the formation of voids in the reactor vessel head while the plant was shutdown and  
  Specification 5.4.1.a for failure to properly implement Procedure AP 14A-003, Scaffold
depressurized in successive refueling outages. This issue and the corrective actions are  
  Construction and Use, when scaffolding was erected against operable safety-related
being tracked by the licensee in Condition Reports 22501, 20648, 20568, and 20633.
  equipment.
Due to the licensees failure to restore compliance from previous  
  Description. On October 15, 2009, the inspectors identified scaffolding in contact with
NCV 05000482/2008004-07 within a reasonable time after the violation was identified,  
  component cooling water piping inside containment. The piping was the containment
this violation is being cited as a Notice of Violation consistent with Section VI.A of the  
  loop which did not have any required cooling loads, but was part of an operating
Enforcement Policy: VIO 05000482/2009005-11, Failure to Correct Vessel Head Vent  
  component cooling water train that was cooling the core. At the time, reactor coolant
Path (EA-10-020).  
  system level was below the vessel flange. The tag on the scaffold explicitly stated that it
.2  
  was not seismically qualified. The inspectors discussed the issue with the shift manager
Introduction. The inspectors identified a Green noncited violation of Technical  
  who immediately had the scaffold moved. Both steam generators were inoperable and
Specification 5.4.1.a for failure to properly implement Procedure AP 14A-003, Scaffold  
  both trains of residual heat removal were required to be operable. The inspectors
Construction and Use, when scaffolding was erected against operable safety-related  
  reviewed the bases for Technical Specification 3.4.7, RCS Loops - Mode 5, Loops
equipment.  
  Filled, which required an operable heat sink path from residual heat removal to
Description. On October 15, 2009, the inspectors identified scaffolding in contact with  
  component cooling water to essential service water.
component cooling water piping inside containment. The piping was the containment  
  Procedure AP 14A-003, Scaffold Construction and Use, step 6.4.15, required
loop which did not have any required cooling loads, but was part of an operating  
  scaffolding to be two inches away from equipment. Attachment F of this procedure
component cooling water train that was cooling the core. At the time, reactor coolant  
  specifies the requirements for seismically qualified scaffolds. The scaffold form stated
system level was below the vessel flange. The tag on the scaffold explicitly stated that it  
  that the scaffolding was required to be removed prior to Mode 4, which was incorrect
was not seismically qualified. The inspectors discussed the issue with the shift manager  
  because it allowed nonseismically qualified scaffold to be installed in the zone of
who immediately had the scaffold moved. Both steam generators were inoperable and  
  influence of operable equipment since seismic qualification is still required for equipment
both trains of residual heat removal were required to be operable. The inspectors  
  required to be operable in Modes 5 and 6. This issue was entered into the corrective
reviewed the bases for Technical Specification 3.4.7, RCS Loops - Mode 5, Loops  
  action program as Condition Report 22464.
Filled, which required an operable heat sink path from residual heat removal to  
  Analysis. The construction of an unqualified scaffold against operable component
component cooling water to essential service water.  
  cooling water piping was a performance deficiency. Traditional enforcement does not
Procedure AP 14A-003, Scaffold Construction and Use, step 6.4.15, required  
  apply since there were no actual safety consequences or potential for impacting the
scaffolding to be two inches away from equipment. Attachment F of this procedure  
  NRC's regulatory function, and the finding was not the result of any willful violation of
specifies the requirements for seismically qualified scaffolds. The scaffold form stated  
  NRC requirements or Wolf Creek procedures. The inspectors determined that this
that the scaffolding was required to be removed prior to Mode 4, which was incorrect  
  finding was more than minor because it is associated with the equipment performance
because it allowed nonseismically qualified scaffold to be installed in the zone of  
  attribute for the Mitigating Systems Cornerstone, and it affected the cornerstone
influence of operable equipment since seismic qualification is still required for equipment  
  objective to ensure the availability, reliability, and capability of systems that respond to
required to be operable in Modes 5 and 6. This issue was entered into the corrective  
  initiating events to prevent undesirable consequences (i.e., core damage). Specifically,
action program as Condition Report 22464.  
                                        - 50 -                                    Enclosure 2
Analysis. The construction of an unqualified scaffold against operable component  
cooling water piping was a performance deficiency. Traditional enforcement does not  
apply since there were no actual safety consequences or potential for impacting the  
NRC's regulatory function, and the finding was not the result of any willful violation of  
NRC requirements or Wolf Creek procedures. The inspectors determined that this  
finding was more than minor because it is associated with the equipment performance  
attribute for the Mitigating Systems Cornerstone, and it affected the cornerstone  
objective to ensure the availability, reliability, and capability of systems that respond to  
initiating events to prevent undesirable consequences (i.e., core damage). Specifically,  


    this issue relates to the availability and reliability examples of the equipment
    performance attribute because a latent failure mechanism was not evaluated. The
    inspectors evaluated the significance of this finding using Inspection Manual
- 51 -
    Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance
    Determination Process Phase 1 Operational Checklists for Both PWRs and BWRs. The
    inspectors determined that Checklist 3 was applicable because the unit was in cold
    shutdown with the refueling cavity level less than 23 feet. Using Appendix G,
    Attachment 1, Checklist 3, Phase 2 analysis was not needed and the finding was of very
Enclosure 2
    low safety significance (Green) because the licensee was able to demonstrate that the
this issue relates to the availability and reliability examples of the equipment  
    seismically unqualified scaffolding would not have resulted in a loss of safety function.
performance attribute because a latent failure mechanism was not evaluated. The  
    The inspectors determined the cause of the finding had a human performance aspect in
inspectors evaluated the significance of this finding using Inspection Manual  
    the area of resources. Specifically, Procedure AP 14A-003 was inadequate because it
Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance  
    had conflicting guidance that allowed seismically unqualified scaffolds in Modes 5 and 6
Determination Process Phase 1 Operational Checklists for Both PWRs and BWRs. The  
    [H.2.c].
inspectors determined that Checklist 3 was applicable because the unit was in cold  
    Enforcement. Technical Specification 5.4.1.a requires that procedures be established,
shutdown with the refueling cavity level less than 23 feet. Using Appendix G,  
    implemented and maintained as recommended in Regulatory Guide 1.33, Appendix A.
Attachment 1, Checklist 3, Phase 2 analysis was not needed and the finding was of very  
    Section 9.a of Appendix A, requires, in part, that maintenance affecting safety-related
low safety significance (Green) because the licensee was able to demonstrate that the  
    equipment be accomplished in accordance with procedures. Procedure AP 14A-003
seismically unqualified scaffolding would not have resulted in a loss of safety function.
    Scaffold Construction and Use, Revision 16, step 6.4.15 required two inches of
The inspectors determined the cause of the finding had a human performance aspect in  
    clearance from safety-related structures. Contrary to the above, from October 14 to 15,
the area of resources. Specifically, Procedure AP 14A-003 was inadequate because it  
    2009, the licensee did not provide two inches of clearance between scaffolding and
had conflicting guidance that allowed seismically unqualified scaffolds in Modes 5 and 6  
    safety-related structures. Specifically, component cooling water Train B was in contact
[H.2.c].  
    with a seismically unqualified scaffold while component cooling water was required to be
Enforcement. Technical Specification 5.4.1.a requires that procedures be established,  
    operable. Because the finding is of very low safety significance and has been entered
implemented and maintained as recommended in Regulatory Guide 1.33, Appendix A.
    into the corrective action program as Condition Report 22464, this violation is being
Section 9.a of Appendix A, requires, in part, that maintenance affecting safety-related  
    treated as a noncited violation, consistent with Section VI.A of the NRC Enforcement
equipment be accomplished in accordance with procedures. Procedure AP 14A-003  
    Policy: NCV 05000482/2009005-12, Unevaluated Scaffold Against Component Cooling
Scaffold Construction and Use, Revision 16, step 6.4.15 required two inches of  
    Water Piping.
clearance from safety-related structures. Contrary to the above, from October 14 to 15,  
1R22 Surveillance Testing (71111.22)
2009, the licensee did not provide two inches of clearance between scaffolding and  
  a. Inspection Scope
safety-related structures. Specifically, component cooling water Train B was in contact  
    The inspectors reviewed the USAR, procedure requirements, and technical
with a seismically unqualified scaffold while component cooling water was required to be  
    specifications to ensure that the seven surveillance activities listed below demonstrated
operable. Because the finding is of very low safety significance and has been entered  
    that the systems, structures, and/or components tested were capable of performing their
into the corrective action program as Condition Report 22464, this violation is being  
    intended safety functions. The inspectors either witnessed or reviewed test data to verify
treated as a noncited violation, consistent with Section VI.A of the NRC Enforcement  
    that the significant surveillance test attributes were adequate to address the following:
Policy: NCV 05000482/2009005-12, Unevaluated Scaffold Against Component Cooling  
    *       Preconditioning
Water Piping.  
    *       Evaluation of testing impact on the plant
1R22 Surveillance Testing (71111.22)
    *       Acceptance criteria
a.  
    *       Test equipment
Inspection Scope  
                                          - 51 -                                  Enclosure 2
The inspectors reviewed the USAR, procedure requirements, and technical  
specifications to ensure that the seven surveillance activities listed below demonstrated  
that the systems, structures, and/or components tested were capable of performing their  
intended safety functions. The inspectors either witnessed or reviewed test data to verify  
that the significant surveillance test attributes were adequate to address the following:  
*  
Preconditioning  
*  
Evaluation of testing impact on the plant  
*  
Acceptance criteria  
*  
Test equipment  


*     Procedures
*     Jumper/lifted lead controls
*     Test data
- 52 -
*     Testing frequency and method demonstrated technical specification operability
*     Test equipment removal
*     Restoration of plant systems
*     Fulfillment of ASME Code requirements
*     Updating of performance indicator data
Enclosure 2
*     Engineering evaluations, root causes, and bases for returning tested systems,
*  
      structures, and components not meeting the test acceptance criteria were correct
Procedures  
*     Reference setting data
*  
*     Annunciators and alarms setpoints
Jumper/lifted lead controls  
The inspectors also verified that licensee personnel identified and implemented any
*  
needed corrective actions associated with the surveillance testing.
Test data  
*     October 28, 2009, MOV 8811A as-found inservice surveillance test
*  
*     August 10, 2009, STS IC-250B, Channel operational test containment
Testing frequency and method demonstrated technical specification operability  
      atmosphere and reactor coolant system leak rate radiation Monitor GT RE-0031
*  
*     November 5, 2009, STS PE-139, Local leak rate test of Penetration 39,
Test equipment removal  
      BB HV-351C
*  
*     September 17, 2009, Train A auxiliary feedwater inservice testing of
Restoration of plant systems  
      Valves ALV0002 and ALV0009
*  
*     November 3, 2009, Essential service water Train B leak test of underground pipe
Fulfillment of ASME Code requirements  
*     September 28, 2009, Emergency Diesel Generator A, 24-hour endurance run
*  
*     October 15, 2009, Emergency Diesel Panel KJ-122/123 safety to nonsafety fuse
Updating of performance indicator data  
      inspections
*  
Specific documents reviewed during this inspection are listed in the attachment.
Engineering evaluations, root causes, and bases for returning tested systems,  
These activities constitute completion of seven surveillance testing inspection samples
structures, and components not meeting the test acceptance criteria were correct  
as defined in Inspection Procedure IP 71111.22-05.
*  
                                    - 52 -                                Enclosure 2
Reference setting data  
*  
Annunciators and alarms setpoints  
The inspectors also verified that licensee personnel identified and implemented any  
needed corrective actions associated with the surveillance testing.
*  
October 28, 2009, MOV 8811A as-found inservice surveillance test  
*  
August 10, 2009, STS IC-250B, Channel operational test containment  
atmosphere and reactor coolant system leak rate radiation Monitor GT RE-0031
*  
November 5, 2009, STS PE-139, Local leak rate test of Penetration 39,  
BB HV-351C  
*  
September 17, 2009, Train A auxiliary feedwater inservice testing of  
Valves ALV0002 and ALV0009
*  
November 3, 2009, Essential service water Train B leak test of underground pipe  
*  
September 28, 2009, Emergency Diesel Generator A, 24-hour endurance run
*  
October 15, 2009, Emergency Diesel Panel KJ-122/123 safety to nonsafety fuse  
inspections
Specific documents reviewed during this inspection are listed in the attachment.  
These activities constitute completion of seven surveillance testing inspection samples  
as defined in Inspection Procedure IP 71111.22-05.  


  b. Findings
      No findings of significance were identified.
2.   RADIATION SAFETY
- 53 -
      Cornerstone: Occupational and Public Radiation Safety
2OS1 Access Control to Radiologically Significant Areas (71121.01)
  a. Inspection Scope
      This area was inspected to assess licensee personnels performance in implementing
      physical and administrative controls for airborne radioactivity areas, radiation areas, high
Enclosure 2
      radiation areas, and worker adherence to these controls. The inspectors used the
b.  
      requirements in 10 CFR Part 20, the technical specifications, and the licensees
Findings  
      procedures required by technical specifications as criteria for determining compliance.
No findings of significance were identified.
      During the inspection, the inspectors interviewed the radiation protection manager,
2.  
      radiation protection supervisors, and radiation workers. The inspectors performed
RADIATION SAFETY  
      independent radiation dose rate measurements and reviewed the following items:
Cornerstone: Occupational and Public Radiation Safety  
      *       Performance indicator events and associated documentation packages reported
              by the licensee in the Occupational Radiation Safety Cornerstone
2OS1 Access Control to Radiologically Significant Areas (71121.01)  
      *       Controls (surveys, posting, and barricades) of radiation, high radiation, or
              airborne radioactivity areas
a.  
      *       Radiation work permits, procedures, engineering controls, and air sampler
Inspection Scope  
              locations
      *       Conformity of electronic personal dosimeter alarm set points with survey
This area was inspected to assess licensee personnels performance in implementing  
              indications and plant policy; workers knowledge of required actions when their
physical and administrative controls for airborne radioactivity areas, radiation areas, high  
              electronic personnel dosimeter noticeably malfunctions or alarms
radiation areas, and worker adherence to these controls. The inspectors used the  
      *       Barrier integrity and performance of engineering controls in airborne radioactivity
requirements in 10 CFR Part 20, the technical specifications, and the licensees  
              areas
procedures required by technical specifications as criteria for determining compliance.
      *       Physical and programmatic controls for highly activated or contaminated
During the inspection, the inspectors interviewed the radiation protection manager,  
              materials (nonfuel) stored within spent fuel and other storage pools
radiation protection supervisors, and radiation workers. The inspectors performed  
      *       Self-assessments, audits, licensee event reports, and special reports related to
independent radiation dose rate measurements and reviewed the following items:  
              the access control program since the last inspection
      *       Corrective action documents related to access controls
*  
      *       Licensee actions in cases of repetitive deficiencies or significant individual
Performance indicator events and associated documentation packages reported  
              deficiencies
by the licensee in the Occupational Radiation Safety Cornerstone  
                                          - 53 -                                    Enclosure 2
*  
Controls (surveys, posting, and barricades) of radiation, high radiation, or  
airborne radioactivity areas  
*  
Radiation work permits, procedures, engineering controls, and air sampler  
locations  
*  
Conformity of electronic personal dosimeter alarm set points with survey  
indications and plant policy; workers knowledge of required actions when their  
electronic personnel dosimeter noticeably malfunctions or alarms  
*  
Barrier integrity and performance of engineering controls in airborne radioactivity  
areas
*  
Physical and programmatic controls for highly activated or contaminated  
materials (nonfuel) stored within spent fuel and other storage pools  
*  
Self-assessments, audits, licensee event reports, and special reports related to  
the access control program since the last inspection  
*  
Corrective action documents related to access controls  
*  
Licensee actions in cases of repetitive deficiencies or significant individual  
deficiencies  


      *       Radiation work permit briefings and worker instructions
      *       Adequacy of radiological controls, such as required surveys, radiation protection
              job coverage, and contamination control during job performance
- 54 -
      *       Dosimetry placement in high radiation work areas with significant dose rate
              gradients
      *       Changes in licensee procedural controls of high dose rate - high radiation areas
              and very high radiation areas
      *       Controls for special areas that have the potential to become very high radiation
Enclosure 2
              areas during certain plant operations
      *       Posting and locking of entrances to all accessible high dose rate - high radiation
*  
              areas and very high radiation areas
Radiation work permit briefings and worker instructions  
      *       Radiation worker and radiation protection technician performance with respect to
              radiation protection work requirements
*  
      Either because the conditions did not exist or an event had not occurred, no
Adequacy of radiological controls, such as required surveys, radiation protection  
      opportunities were available to review the following items:
job coverage, and contamination control during job performance  
      *       Adequacy of the licensees internal dose assessment for any actual internal
              exposure greater than 50 millirem committed effective dose equivalent
*  
      These activities constitute completion of 21 of the required 21 samples as defined in
Dosimetry placement in high radiation work areas with significant dose rate  
      Inspection Procedure IP 71121.01-05.
gradients  
  b. Findings
.1   Introduction. The inspector identified a Green noncited violation of
*  
      Technical Specification 5.7.2.a.1 for failure to maintain administrative control of door
Changes in licensee procedural controls of high dose rate - high radiation areas  
      and gate keys to high radiation areas with dose rates greater than 1 rem per hour but
and very high radiation areas  
      less than 500 rads per hour (referred to as locked high radiation areas).
      Description. During a review of the licensees program for administrative control of
*  
      keys to doors and gates to locked high radiation areas and very high radiation areas, the
Controls for special areas that have the potential to become very high radiation  
      inspector found that the health physics department had a master key to locked high
areas during certain plant operations  
      radiation areas. This key was not controlled in accordance with licensee
      Procedure AP 25A-200, Access to Locked High or Very High Radiation Areas,
*  
      Revision 20, which stated that site security was responsible for issuing locked high
Posting and locking of entrances to all accessible high dose rate - high radiation  
      radiation area and very high radiation area keys. In accordance with technical
areas and very high radiation areas  
      specifications, health physics management designated the site security department to
      administratively (and procedurally) control the keys. Although site security was
*  
      effectively meeting the procedure requirement for issuing all other locked and very high
Radiation worker and radiation protection technician performance with respect to  
                                          - 54 -                                  Enclosure 2
radiation protection work requirements  
Either because the conditions did not exist or an event had not occurred, no  
opportunities were available to review the following items:  
*  
Adequacy of the licensees internal dose assessment for any actual internal  
exposure greater than 50 millirem committed effective dose equivalent  
These activities constitute completion of 21 of the required 21 samples as defined in  
Inspection Procedure IP 71121.01-05.  
b.  
Findings  
.1  
Introduction. The inspector identified a Green noncited violation of  
Technical Specification 5.7.2.a.1 for failure to maintain administrative control of door  
and gate keys to high radiation areas with dose rates greater than 1 rem per hour but  
less than 500 rads per hour (referred to as locked high radiation areas).  
Description. During a review of the licensees program for administrative control of  
keys to doors and gates to locked high radiation areas and very high radiation areas, the  
inspector found that the health physics department had a master key to locked high  
radiation areas. This key was not controlled in accordance with licensee
Procedure AP 25A-200, Access to Locked High or Very High Radiation Areas,  
Revision 20, which stated that site security was responsible for issuing locked high  
radiation area and very high radiation area keys. In accordance with technical  
specifications, health physics management designated the site security department to  
administratively (and procedurally) control the keys. Although site security was  
effectively meeting the procedure requirement for issuing all other locked and very high  


    radiation area keys, site security was unaware that the health physics department had
    the only master key to locked high radiation areas at the site. By procedure, site security
    administratively controlled the other keys (to locked and very high radiation areas) by
- 55 -
    maintaining an inventory of them, performing physical inventories of the keys each shift,
    and labeling the keys. None of these administrative controls were implemented for the
    master key in the health physics department. The licensee immediately documented the
    deficiency in a condition report and implemented temporary administrative controls until
    a permanent disposition for the master key had been identified.
Enclosure 2
    Analysis. Failure to maintain administrative control of the master key to locked high
radiation area keys, site security was unaware that the health physics department had  
    radiation areas was a performance deficiency. This finding is greater than minor because if
the only master key to locked high radiation areas at the site. By procedure, site security  
    left uncorrected the finding has the potential to lead to a more significant safety concern in
administratively controlled the other keys (to locked and very high radiation areas) by  
    that an individual could receive unanticipated radiation dose by gaining access a locked high
maintaining an inventory of them, performing physical inventories of the keys each shift,  
    radiation area without the proper controls and briefing. This finding was evaluated using
and labeling the keys. None of these administrative controls were implemented for the  
    Inspection Manual Chapter 0609, Significance Determination Process, Appendix C,
master key in the health physics department. The licensee immediately documented the  
    Occupational Radiation Safety Significance Determination Process, and was determined to
deficiency in a condition report and implemented temporary administrative controls until  
    be of very low safety significance because it did not involve: (1) an as low as is reasonably
a permanent disposition for the master key had been identified.  
    achievable (ALARA) planning or work control issue, (2) an overexposure, (3) a substantial
Analysis. Failure to maintain administrative control of the master key to locked high  
    potential for overexposure, or (4) an impaired ability to assess dose. Additionally, the
radiation areas was a performance deficiency. This finding is greater than minor because if  
    violation has a crosscutting aspect in the area of human performance associated with the
left uncorrected the finding has the potential to lead to a more significant safety concern in  
    work practices component because the lack of peer and self-checking resulted in
that an individual could receive unanticipated radiation dose by gaining access a locked high  
    inadequate control of keys to locked high radiation areas [H.4(a)].
radiation area without the proper controls and briefing. This finding was evaluated using  
    Enforcement. Technical Specification 5.7.2.a.1 requires, in part, that each entryway to a
Inspection Manual Chapter 0609, Significance Determination Process, Appendix C,  
    high radiation area with dose rates greater than 1.0 rem per hour but less than 500 rads
Occupational Radiation Safety Significance Determination Process, and was determined to  
    per hour shall be provided with a locked or continuously guarded door or gate that
be of very low safety significance because it did not involve: (1) an as low as is reasonably  
    prevents unauthorized entry and all keys shall be maintained under the administrative
achievable (ALARA) planning or work control issue, (2) an overexposure, (3) a substantial  
    control of the shift manager/control room supervisor, health physics supervision, or
potential for overexposure, or (4) an impaired ability to assess dose. Additionally, the  
    his/her designee. Contrary to the above, as of October 21, 2009, the licensee failed to
violation has a crosscutting aspect in the area of human performance associated with the  
    maintain administrative control of a master key to high radiation areas with dose rates in
work practices component because the lack of peer and self-checking resulted in  
    excess of 1.0 rem per hour but less than 500 rads per hour. Because this violation was
inadequate control of keys to locked high radiation areas [H.4(a)].  
    of very low safety significance and has been entered into the licensee's corrective action
Enforcement. Technical Specification 5.7.2.a.1 requires, in part, that each entryway to a  
    program as Condition Report 20973, it is being treated as a noncited violation consistent
high radiation area with dose rates greater than 1.0 rem per hour but less than 500 rads  
    with Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-13, Failure
per hour shall be provided with a locked or continuously guarded door or gate that  
    to Maintain Administrative Control of Keys to Locked High Radiation Areas.
prevents unauthorized entry and all keys shall be maintained under the administrative  
2OS2 ALARA Planning and Controls (71121.02)
control of the shift manager/control room supervisor, health physics supervision, or  
  a. Inspection Scope
his/her designee. Contrary to the above, as of October 21, 2009, the licensee failed to  
    The inspectors assessed licensee personnels performance with respect to maintaining
maintain administrative control of a master key to high radiation areas with dose rates in  
    individual and collective radiation exposures as low as is reasonably achievable. The
excess of 1.0 rem per hour but less than 500 rads per hour. Because this violation was  
    inspectors used the requirements in 10 CFR Part 20 and the licensees procedures
of very low safety significance and has been entered into the licensee's corrective action  
    required by technical specifications as criteria for determining compliance. The
program as Condition Report 20973, it is being treated as a noncited violation consistent  
    inspectors interviewed licensee personnel and reviewed the following:
with Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-13, Failure  
                                          - 55 -                                  Enclosure 2
to Maintain Administrative Control of Keys to Locked High Radiation Areas.  
2OS2 ALARA Planning and Controls (71121.02)  
a.  
Inspection Scope  
The inspectors assessed licensee personnels performance with respect to maintaining  
individual and collective radiation exposures as low as is reasonably achievable. The  
inspectors used the requirements in 10 CFR Part 20 and the licensees procedures  
required by technical specifications as criteria for determining compliance. The  
inspectors interviewed licensee personnel and reviewed the following:  


  *     Five outage or on-line maintenance work activities scheduled during the
          inspection period and associated work activity exposure estimates which were
          likely to result in the highest personnel collective exposures
- 56 -
  *     Site-specific ALARA procedures
  *     ALARA work activity evaluations, exposure estimates, and exposure mitigation
          requirements
  *     Interfaces between operations, radiation protection, maintenance, maintenance
          planning, scheduling and engineering groups
Enclosure 2
  *     Shielding requests and dose/benefit analyses
*  
  *     Dose rate reduction activities in work planning
Five outage or on-line maintenance work activities scheduled during the  
  *     Use of engineering controls to achieve dose reductions and dose reduction
inspection period and associated work activity exposure estimates which were  
          benefits afforded by shielding
likely to result in the highest personnel collective exposures  
  *     Workers use of the low dose waiting areas
  *     First-line job supervisors contribution to ensuring work activities are conducted in
*  
          a dose efficient manner
Site-specific ALARA procedures  
  *     Radiation worker and radiation protection technician performance during work
          activities in radiation areas, airborne radioactivity areas, or high radiation areas
*  
  *     Self-assessments, audits, and special reports related to the ALARA program
ALARA work activity evaluations, exposure estimates, and exposure mitigation  
          since the last inspection
requirements  
  *     Corrective action documents related to the ALARA program and follow-up
          activities, such as initial problem identification, characterization, and tracking
*  
  Specific documents reviewed during this inspection are listed in the attachment.
Interfaces between operations, radiation protection, maintenance, maintenance  
  These activities constitute completion of 6 of the required 15 samples and 6 of the
planning, scheduling and engineering groups  
  optional samples as defined in Inspection Procedure IP 71121.02-05.
b. Findings
*  
  No findings of significance were identified.
Shielding requests and dose/benefit analyses  
                                          - 56 -                                  Enclosure 2
*  
Dose rate reduction activities in work planning  
*  
Use of engineering controls to achieve dose reductions and dose reduction  
benefits afforded by shielding  
*  
Workers use of the low dose waiting areas  
*  
First-line job supervisors contribution to ensuring work activities are conducted in  
a dose efficient manner  
*  
Radiation worker and radiation protection technician performance during work  
activities in radiation areas, airborne radioactivity areas, or high radiation areas
*  
Self-assessments, audits, and special reports related to the ALARA program  
since the last inspection  
*  
Corrective action documents related to the ALARA program and follow-up  
activities, such as initial problem identification, characterization, and tracking  
Specific documents reviewed during this inspection are listed in the attachment.  
These activities constitute completion of 6 of the required 15 samples and 6 of the  
optional samples as defined in Inspection Procedure IP 71121.02-05.  
b.  
Findings  
No findings of significance were identified.  


4.   OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
.1   Data Submission Issue
- 57 -
  a. Inspection Scope
      The inspectors performed a review of the data submitted by the licensee for the 3rd
      Quarter 2009 performance indicators for any obvious inconsistencies prior to its public
      release in accordance with Inspection Manual Chapter 0608, Performance Indicator
      Program.
Enclosure 2
      This review was performed as part of the inspectors normal plant status activities and,
4.  
      as such, did not constitute a separate inspection sample.
OTHER ACTIVITIES  
  b. Findings
4OA1 Performance Indicator Verification (71151)  
      No findings of significance were identified.
.1  
.2   Mitigating Systems Performance Index - Emergency ac Power System
Data Submission Issue  
  a. Inspection Scope
a.  
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
Inspection Scope  
      Index - Emergency ac Power System performance indicator data for the period from the
The inspectors performed a review of the data submitted by the licensee for the 3rd  
      4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the
Quarter 2009 performance indicators for any obvious inconsistencies prior to its public  
      performance indicator data reported during those periods, performance indicator
release in accordance with Inspection Manual Chapter 0608, Performance Indicator  
      definitions and guidance contained in Revision 6 of the Nuclear Energy Institute (NEI)
Program.  
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, were
This review was performed as part of the inspectors normal plant status activities and,  
      used. The inspectors reviewed the licensees operator narrative logs, mitigating systems
as such, did not constitute a separate inspection sample.
      performance index derivation reports, issue reports, event reports, and NRC integrated
b.  
      inspection reports for the period of October 1, 2008, through September 30, 2009, to
Findings  
      validate the accuracy of the submittals. The inspectors reviewed the mitigating systems
No findings of significance were identified.
      performance index component risk coefficient to determine if it had changed by more
.2  
      than 25 percent in value since the previous inspection, and if so, that the change was in
Mitigating Systems Performance Index - Emergency ac Power System  
      accordance with applicable NEI guidance. The inspectors also reviewed the licensees
a.  
      issue report database to determine if any problems had been identified with the
Inspection Scope  
      performance indicator data collected or transmitted for this indicator and none were
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
      identified. Specific documents reviewed are described in the attachment to this report.
Index - Emergency ac Power System performance indicator data for the period from the  
      This inspection constitutes one mitigating systems performance index - emergency ac
4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the  
      power system sample as defined by Inspection Procedure IP 71151.
performance indicator data reported during those periods, performance indicator  
  b. Findings
definitions and guidance contained in Revision 6 of the Nuclear Energy Institute (NEI)  
      No findings of significance were identified.
Document 99-02, Regulatory Assessment Performance Indicator Guideline, were  
                                          - 57 -                                  Enclosure 2
used. The inspectors reviewed the licensees operator narrative logs, mitigating systems  
performance index derivation reports, issue reports, event reports, and NRC integrated  
inspection reports for the period of October 1, 2008, through September 30, 2009, to  
validate the accuracy of the submittals. The inspectors reviewed the mitigating systems  
performance index component risk coefficient to determine if it had changed by more  
than 25 percent in value since the previous inspection, and if so, that the change was in  
accordance with applicable NEI guidance. The inspectors also reviewed the licensees  
issue report database to determine if any problems had been identified with the  
performance indicator data collected or transmitted for this indicator and none were  
identified. Specific documents reviewed are described in the attachment to this report.  
This inspection constitutes one mitigating systems performance index - emergency ac  
power system sample as defined by Inspection Procedure IP 71151.  
b.  
Findings  
No findings of significance were identified.  


.3   Mitigating Systems Performance Index - High Pressure Injection Systems
  a. Inspection Scope
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
- 58 -
      Index - High Pressure Injection Systems performance indicator data for the period from
      the 4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the
      performance indicator data reported during those periods, performance indicator
      definitions and guidance contained in Revision 6 of the NEI Document 99-02,
      Regulatory Assessment Performance Indicator Guideline, were used. The inspectors
Enclosure 2
      reviewed the licensees operator narrative logs, issue reports, mitigating systems
.3  
      performance index derivation reports, event reports, and NRC integrated inspection
Mitigating Systems Performance Index - High Pressure Injection Systems  
      reports for the period of October 1, 2008, through September 30, 2009, to validate the
a.  
      accuracy of the submittals. The inspectors reviewed the mitigating systems performance
Inspection Scope  
      index component risk coefficient to determine if it had changed by more than 25 percent
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
      in value since the previous inspection, and if so, that the change was in accordance with
Index - High Pressure Injection Systems performance indicator data for the period from  
      applicable NEI guidance. The inspectors also reviewed the licensees issue report
the 4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the  
      database to determine if any problems had been identified with the performance
performance indicator data reported during those periods, performance indicator  
      indicator data collected or transmitted for this indicator and none were identified.
definitions and guidance contained in Revision 6 of the NEI Document 99-02,  
      Specific documents reviewed are described in the attachment to this report.
Regulatory Assessment Performance Indicator Guideline, were used. The inspectors  
      This inspection constitutes one mitigating systems performance index - high pressure
reviewed the licensees operator narrative logs, issue reports, mitigating systems  
      injection system sample as defined by Inspection Procedure IP 71151.
performance index derivation reports, event reports, and NRC integrated inspection  
  b. Findings
reports for the period of October 1, 2008, through September 30, 2009, to validate the  
      No findings of significance were identified.
accuracy of the submittals. The inspectors reviewed the mitigating systems performance  
.4   Mitigating Systems Performance Index - Auxiliary Feedwater System
index component risk coefficient to determine if it had changed by more than 25 percent  
  a. Inspection Scope
in value since the previous inspection, and if so, that the change was in accordance with  
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
applicable NEI guidance. The inspectors also reviewed the licensees issue report  
      Index - Auxiliary Feedwater System performance indicator data for the period from the
database to determine if any problems had been identified with the performance  
      4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the
indicator data collected or transmitted for this indicator and none were identified.  
      performance indicator data reported during those periods, performance indicator
Specific documents reviewed are described in the attachment to this report.
      definitions and guidance contained in Revision 6 of the NEI Document 99-02,
This inspection constitutes one mitigating systems performance index - high pressure  
      Regulatory Assessment Performance Indicator Guideline, were used. The inspectors
injection system sample as defined by Inspection Procedure IP 71151.  
      reviewed the licensees operator narrative logs, issue reports, event reports, mitigating
b.  
      systems performance index derivation reports, and NRC integrated inspection reports
Findings  
      for the period of October 1, 2008, through September 30, 2009, to validate the accuracy
No findings of significance were identified.  
      of the submittals. The inspectors reviewed the mitigating systems performance index
.4  
      component risk coefficient to determine if it had changed by more than 25 percent in
Mitigating Systems Performance Index - Auxiliary Feedwater System  
      value since the previous inspection, and if so, that the change was in accordance with
a.  
      applicable NEI guidance. The inspectors also reviewed the licensees issue report
Inspection Scope  
      database to determine if any problems had been identified with the performance
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
      indicator data collected or transmitted for this indicator and none were identified.
Index - Auxiliary Feedwater System performance indicator data for the period from the  
      Specific documents reviewed are described in the attachment to this report.
4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the  
                                          - 58 -                                  Enclosure 2
performance indicator data reported during those periods, performance indicator  
definitions and guidance contained in Revision 6 of the NEI Document 99-02,  
Regulatory Assessment Performance Indicator Guideline, were used. The inspectors  
reviewed the licensees operator narrative logs, issue reports, event reports, mitigating  
systems performance index derivation reports, and NRC integrated inspection reports  
for the period of October 1, 2008, through September 30, 2009, to validate the accuracy  
of the submittals. The inspectors reviewed the mitigating systems performance index  
component risk coefficient to determine if it had changed by more than 25 percent in  
value since the previous inspection, and if so, that the change was in accordance with  
applicable NEI guidance. The inspectors also reviewed the licensees issue report  
database to determine if any problems had been identified with the performance  
indicator data collected or transmitted for this indicator and none were identified.
Specific documents reviewed are described in the attachment to this report.


      This inspection constitutes one mitigating systems performance index - auxiliary
      feedwater sample as defined by Inspection Procedure IP 71151.
  b. Findings
- 59 -
      No findings of significance were identified.
.5   Mitigating Systems Performance Index - Residual Heat Removal System
  a. Inspection Scope
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
      Index - Residual Heat Removal System performance indicator data for the period from
Enclosure 2
      the 4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the
This inspection constitutes one mitigating systems performance index - auxiliary  
      performance indicator data reported during those periods, performance indicator
feedwater sample as defined by Inspection Procedure IP 71151.  
      definitions and guidance contained in Revision 6 of the NEI Document 99-02,
b.  
      Regulatory Assessment Performance Indicator Guideline, were used. The inspectors
Findings  
      reviewed the licensees operator narrative logs, issue reports, mitigating systems
No findings of significance were identified.  
      performance index derivation reports, event reports, and NRC integrated inspection
.5  
      reports for the period of October 1, 2008, through September 30, 2009, to validate the
Mitigating Systems Performance Index - Residual Heat Removal System  
      accuracy of the submittals. The inspectors reviewed the mitigating systems
a.  
      performance index component risk coefficient to determine if it had changed by more
Inspection Scope  
      than 25 percent in value since the previous inspection, and if so, that the change was in
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
      accordance with applicable NEI guidance. The inspectors also reviewed the licensees
Index - Residual Heat Removal System performance indicator data for the period from  
      issue report database to determine if any problems had been identified with the
the 4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the  
      performance indicator data collected or transmitted for this indicator and none were
performance indicator data reported during those periods, performance indicator  
      identified. Specific documents reviewed are described in the attachment to this report.
definitions and guidance contained in Revision 6 of the NEI Document 99-02,  
      This inspection constitutes one Mitigating Systems Performance Index - Residual Heat
Regulatory Assessment Performance Indicator Guideline, were used. The inspectors  
      Removal System sample as defined by Inspection Procedure IP 71151.
reviewed the licensees operator narrative logs, issue reports, mitigating systems  
  b. Findings
performance index derivation reports, event reports, and NRC integrated inspection  
      No findings of significance were identified.
reports for the period of October 1, 2008, through September 30, 2009, to validate the  
.6   Mitigating Systems Performance Index - Cooling Water Systems
accuracy of the submittals. The inspectors reviewed the mitigating systems  
  a. Inspection Scope
performance index component risk coefficient to determine if it had changed by more  
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
than 25 percent in value since the previous inspection, and if so, that the change was in  
      Index - Cooling Water Systems performance indicator data for the period from the 4th
accordance with applicable NEI guidance. The inspectors also reviewed the licensees  
      quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the
issue report database to determine if any problems had been identified with the  
      performance indicator data reported during those periods, performance indicator
performance indicator data collected or transmitted for this indicator and none were  
      definitions and guidance contained in Revision 6 of the NEI Document 99-02,
identified. Specific documents reviewed are described in the attachment to this report.
      Regulatory Assessment Performance Indicator Guideline, were used. The inspectors
This inspection constitutes one Mitigating Systems Performance Index - Residual Heat  
      reviewed the licensees operator narrative logs, issue reports, mitigating systems
Removal System sample as defined by Inspection Procedure IP 71151.  
      performance index derivation reports, event reports, and NRC integrated inspection
b.  
      reports for the period of October 1, 2008, to September 30, 2009, to validate the
Findings  
                                        - 59 -                                    Enclosure 2
No findings of significance were identified.  
.6  
Mitigating Systems Performance Index - Cooling Water Systems  
a.  
Inspection Scope  
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
Index - Cooling Water Systems performance indicator data for the period from the 4th  
quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the  
performance indicator data reported during those periods, performance indicator  
definitions and guidance contained in Revision 6 of the NEI Document 99-02,  
Regulatory Assessment Performance Indicator Guideline, were used. The inspectors  
reviewed the licensees operator narrative logs, issue reports, mitigating systems  
performance index derivation reports, event reports, and NRC integrated inspection  
reports for the period of October 1, 2008, to September 30, 2009, to validate the  


      accuracy of the submittals. The inspectors reviewed the mitigating systems
      performance index component risk coefficient to determine if it had changed by more
      than 25 percent in value since the previous inspection, and if so, that the change was in
- 60 -
      accordance with applicable NEI guidance. The inspectors also reviewed the licensees
      issue report database to determine if any problems had been identified with the
      performance indicator data collected or transmitted for this indicator and none were
      identified. Specific documents reviewed are described in the attachment to this report.
      This inspection constitutes one mitigating systems performance index - cooling water
Enclosure 2
      system sample as defined by Inspection Procedure IP 71151.
accuracy of the submittals. The inspectors reviewed the mitigating systems  
  b. Findings
performance index component risk coefficient to determine if it had changed by more  
      No findings of significance were identified.
than 25 percent in value since the previous inspection, and if so, that the change was in  
.7   Occupational Exposure Control Effectiveness (OR01)
accordance with applicable NEI guidance. The inspectors also reviewed the licensees  
  a. Inspection Scope
issue report database to determine if any problems had been identified with the  
      The inspectors sampled licensee submittals for the Occupational Radiological
performance indicator data collected or transmitted for this indicator and none were  
      Occurrences performance indicator for the period from the 4th quarter 2008 through 3rd
identified. Specific documents reviewed are described in the attachment to this report.  
      quarter 2009. To determine the accuracy of the performance indicator data reported
This inspection constitutes one mitigating systems performance index - cooling water  
      during those periods, performance indicator definitions and guidance contained in NEI
system sample as defined by Inspection Procedure IP 71151.  
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,
b.  
      was used. The inspectors reviewed the licensees assessment of the performance
Findings  
      indicator for occupational radiation safety to determine if indicator related data was
No findings of significance were identified.  
      adequately assessed and reported. To assess the adequacy of the licensees
.7  
      performance indicator data collection and analyses, the inspectors discussed with
Occupational Exposure Control Effectiveness (OR01)  
      radiation protection staff, the scope and breadth of its data review, and the results of
      those reviews. The inspectors independently reviewed electronic dosimetry dose rate
a.  
      and accumulated dose alarm and dose reports and the dose assignments for any
Inspection Scope  
      intakes that occurred during the time period reviewed to determine if there were
      potentially unrecognized occurrences. The inspectors also conducted walkdowns of
The inspectors sampled licensee submittals for the Occupational Radiological  
      numerous locked high and very high radiation area entrances to determine the adequacy
Occurrences performance indicator for the period from the 4th quarter 2008 through 3rd  
      of the controls in place for these areas.
quarter 2009. To determine the accuracy of the performance indicator data reported  
      These activities constitute completion of the occupational radiological occurrences
during those periods, performance indicator definitions and guidance contained in NEI  
      sample as defined in Inspection Procedure IP 71151-05.
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,  
  b. Findings
was used. The inspectors reviewed the licensees assessment of the performance  
      No findings of significance were identified.
indicator for occupational radiation safety to determine if indicator related data was  
                                          - 60 -                                  Enclosure 2
adequately assessed and reported. To assess the adequacy of the licensees  
performance indicator data collection and analyses, the inspectors discussed with  
radiation protection staff, the scope and breadth of its data review, and the results of  
those reviews. The inspectors independently reviewed electronic dosimetry dose rate  
and accumulated dose alarm and dose reports and the dose assignments for any  
intakes that occurred during the time period reviewed to determine if there were  
potentially unrecognized occurrences. The inspectors also conducted walkdowns of  
numerous locked high and very high radiation area entrances to determine the adequacy  
of the controls in place for these areas.  
These activities constitute completion of the occupational radiological occurrences  
sample as defined in Inspection Procedure IP 71151-05.  
b.  
Findings  
No findings of significance were identified.  


.8   Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual
      Radiological Effluent Occurrences (PR01)
  a. Inspection Scope
- 61 -
      The inspectors sampled licensee submittals for the Radiological Effluent Technical
      Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences
      performance indicator for the period from the 4th quarter 2008 through 3rd quarter 2009.
      To determine the accuracy of the performance indicator data reported during those
      periods, performance indicator definitions and guidance contained in NEI
Enclosure 2
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,
.8  
      was used. The inspectors reviewed the licensees issue report database and selected
Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual  
      individual reports generated since this indicator was last reviewed to identify any
Radiological Effluent Occurrences (PR01)  
      potential occurrences such as unmonitored, uncontrolled, or improperly calculated
      effluent releases that may have impacted offsite dose.
a.  
      These activities constitute completion of the radiological effluent technical
Inspection Scope  
      specifications/offsite dose calculation manual radiological effluent occurrences sample
      as defined in Inspection Procedure IP 71151-05.
The inspectors sampled licensee submittals for the Radiological Effluent Technical  
  b. Findings
Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences  
      No findings of significance were identified.
performance indicator for the period from the 4th quarter 2008 through 3rd quarter 2009.
4OA2 Identification and Resolution of Problems (71152)
To determine the accuracy of the performance indicator data reported during those  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
periods, performance indicator definitions and guidance contained in NEI  
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,  
      Protection
was used. The inspectors reviewed the licensees issue report database and selected  
.1   Routine Review of Identification and Resolution of Problems
individual reports generated since this indicator was last reviewed to identify any  
  a. Inspection Scope
potential occurrences such as unmonitored, uncontrolled, or improperly calculated  
      As part of the various baseline inspection procedures discussed in previous sections of
effluent releases that may have impacted offsite dose.  
      this report, the inspectors routinely reviewed issues during baseline inspection activities
      and plant status reviews to verify that they were being entered into the licensees
These activities constitute completion of the radiological effluent technical  
      corrective action program at an appropriate threshold, that adequate attention was being
specifications/offsite dose calculation manual radiological effluent occurrences sample  
      given to timely corrective actions, and that adverse trends were identified and
as defined in Inspection Procedure IP 71151-05.  
      addressed. The inspectors reviewed attributes that included: the complete and
      accurate identification of the problem; the timely correction, commensurate with the
b.  
      safety significance; the evaluation and disposition of performance issues, generic
Findings  
      implications, common causes, contributing factors, root causes, extent of condition
      reviews, and previous occurrences reviews; and the classification, prioritization, focus,
No findings of significance were identified.  
      and timeliness of corrective actions. Minor issues entered into the licensees corrective
      action program because of the inspectors observations are included in the attached list
4OA2 Identification and Resolution of Problems (71152)
      of documents reviewed.
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
                                          - 61 -                                  Enclosure 2
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical  
Protection  
.1  
Routine Review of Identification and Resolution of Problems  
a.  
Inspection Scope  
As part of the various baseline inspection procedures discussed in previous sections of  
this report, the inspectors routinely reviewed issues during baseline inspection activities  
and plant status reviews to verify that they were being entered into the licensees  
corrective action program at an appropriate threshold, that adequate attention was being  
given to timely corrective actions, and that adverse trends were identified and  
addressed. The inspectors reviewed attributes that included: the complete and  
accurate identification of the problem; the timely correction, commensurate with the  
safety significance; the evaluation and disposition of performance issues, generic  
implications, common causes, contributing factors, root causes, extent of condition  
reviews, and previous occurrences reviews; and the classification, prioritization, focus,  
and timeliness of corrective actions. Minor issues entered into the licensees corrective  
action program because of the inspectors observations are included in the attached list  
of documents reviewed.  


      These routine reviews for the identification and resolution of problems did not constitute
      any additional inspection samples. Instead, by inspection procedure, they were
      considered an integral part of the inspections performed during the quarter and
- 62 -
      documented in Section 1 of this report.
  b. Findings
      No findings of significance were identified.
.2   Daily Corrective Action Program Reviews
  a. Inspection Scope
Enclosure 2
      In order to assist with the identification of repetitive equipment failures and specific
These routine reviews for the identification and resolution of problems did not constitute  
      human performance issues for followup, the inspectors performed a daily screening of
any additional inspection samples. Instead, by inspection procedure, they were  
      items entered into the licensees corrective action program. The inspectors
considered an integral part of the inspections performed during the quarter and  
      accomplished this through review of the stations daily corrective action documents.
documented in Section 1 of this report.  
      The inspectors performed these daily reviews as part of their daily plant status
b.  
      monitoring activities and, as such, did not constitute any separate inspection samples.
Findings  
  b. Findings
No findings of significance were identified.  
      No findings of significance were identified.
.2  
.3   Semi-Annual Trend Review
Daily Corrective Action Program Reviews  
  a. Inspection Scope
a.  
      The inspectors performed a review of the licensees corrective action program and
Inspection Scope  
      associated documents to identify trends that could indicate the existence of a more
In order to assist with the identification of repetitive equipment failures and specific  
      significant safety issue. The inspectors focused their review on repetitive equipment
human performance issues for followup, the inspectors performed a daily screening of  
      issues, but also considered the results of daily corrective action item screening
items entered into the licensees corrective action program. The inspectors  
      discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human
accomplished this through review of the stations daily corrective action documents.  
      performance results. The inspectors nominally considered the 6-month period of
The inspectors performed these daily reviews as part of their daily plant status  
      June 30 through December 31, 2009, although some examples expanded beyond those
monitoring activities and, as such, did not constitute any separate inspection samples.  
      dates where the scope of the trend warranted.
b.  
      The inspectors also included issues documented outside the normal corrective action
Findings  
      program in major equipment problem lists, repetitive and/or rework maintenance lists,
No findings of significance were identified.  
      departmental problem/challenges lists, system health reports, quality assurance
.3  
      audit/surveillance reports, self-assessment reports, and maintenance rule assessments.
Semi-Annual Trend Review  
      The inspectors compared and contrasted their results with the results contained in the
a.  
      licensees corrective action program trending reports. Corrective actions associated with
Inspection Scope  
      a sample of the issues identified in the licensees trending reports were reviewed for
The inspectors performed a review of the licensees corrective action program and  
      adequacy.
associated documents to identify trends that could indicate the existence of a more  
      These activities constitute completion of one single semi-annual trend inspection sample
significant safety issue. The inspectors focused their review on repetitive equipment  
      as defined in Inspection Procedure IP 71152-05.
issues, but also considered the results of daily corrective action item screening  
                                            - 62 -                                  Enclosure 2
discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human  
performance results. The inspectors nominally considered the 6-month period of  
June 30 through December 31, 2009, although some examples expanded beyond those  
dates where the scope of the trend warranted.  
The inspectors also included issues documented outside the normal corrective action  
program in major equipment problem lists, repetitive and/or rework maintenance lists,  
departmental problem/challenges lists, system health reports, quality assurance  
audit/surveillance reports, self-assessment reports, and maintenance rule assessments.
The inspectors compared and contrasted their results with the results contained in the  
licensees corrective action program trending reports. Corrective actions associated with  
a sample of the issues identified in the licensees trending reports were reviewed for  
adequacy.  
These activities constitute completion of one single semi-annual trend inspection sample  
as defined in Inspection Procedure IP 71152-05.  


  b. Findings
      No findings of significance were identified.
.4   Selected Issue Follow-up Inspection
- 63 -
  a. Inspection Scope
      The inspectors selected two issues for follow-up inspection per Inspection
      Procedure IP 71152. During a review of items entered in the licensees corrective action
      program, the inspectors recognized a corrective action item documenting a problem with
      extraction steam on June 23, 2009, that caused an increase in reactivity. The inspectors
Enclosure 2
      reviewed corrective actions and new procedure changes for level control of high
b.  
      pressure feedwater heaters. The inspectors also reviewed several condition reports and
Findings  
      interviewed personnel pertaining to the intermediate range nuclear instrument NI-36.
No findings of significance were identified.  
      The deficiencies associated with NI-36 constituted one in-depth review of an operator
.4  
      work-around.
Selected Issue Follow-up Inspection  
      These activities constitute completion of two in-depth problem identification and
a.  
      resolution samples as defined in Inspection Procedure IP 71152-05.
Inspection Scope  
  b. Findings
The inspectors selected two issues for follow-up inspection per Inspection  
      Introduction. On December 30, 2009, the inspectors identified a Green noncited
Procedure IP 71152. During a review of items entered in the licensees corrective action  
      violation of Technical Specification, Table 3.3.1-1, Function 18.a, when Wolf Creek
program, the inspectors recognized a corrective action item documenting a problem with  
      restarted from on May 18, 2005.
extraction steam on June 23, 2009, that caused an increase in reactivity. The inspectors  
      Description. On April 9, 2005, Wolf Creek shut down for Refueling Outage 14. The
reviewed corrective actions and new procedure changes for level control of high  
      inspectors found no control room log entries stating that source range instrument NI-32
pressure feedwater heaters. The inspectors also reviewed several condition reports and  
      had to be manually energized. The inspectors reviewed a completed copy of
interviewed personnel pertaining to the intermediate range nuclear instrument NI-36.
      STN IC-236, Revision 4, dated April 9, 2005, which stated that compensation voltage
The deficiencies associated with NI-36 constituted one in-depth review of an operator  
      and current were found within tolerance and were left as-found. At the end of Refueling
work-around.  
      Outage 14, in Mode 3, NI-36 indication deviated from indication from intermediate range
These activities constitute completion of two in-depth problem identification and  
      detector NI-35. During interviews with licensed operators, when shutdown banks were
resolution samples as defined in Inspection Procedure IP 71152-05.  
      withdrawn, NI-36 went above 6 E-11 amps and cleared the P-6 interlock while the
b.  
      reactor was subcritical. Indication above 6E-11 normally means the reactor is critical.
Findings  
      The source ranges count rates and NI-35 also increased, but did not indicate criticality.
Introduction. On December 30, 2009, the inspectors identified a Green noncited  
      Troubleshooting was performed under Work Order 05-272906-000 was performed on
violation of Technical Specification, Table 3.3.1-1, Function 18.a, when Wolf Creek  
      May 16, 2005. Instrumentation and controls technicians disconnected, cleaned, and
restarted from on May 18, 2005.  
      reconnected NI-36 cables. The NI-36 cables were then disconnected and reconnected
Description. On April 9, 2005, Wolf Creek shut down for Refueling Outage 14. The  
      two more times. Work Order 05-272906-000 was also used to perform STS IC-436,
inspectors found no control room log entries stating that source range instrument NI-32  
      Channel Calibration NIS Intermediate Range N-36, Revision 15, test the log current
had to be manually energized. The inspectors reviewed a completed copy of  
      amplifier and indicator calibrations, Work Order 05-272906-000 was also used to
STN IC-236, Revision 4, dated April 9, 2005, which stated that compensation voltage  
      perform STN IC-236, Intermediate Range N36 Compensation Voltage Adjustment,
and current were found within tolerance and were left as-found. At the end of Refueling  
      Revision 4 to calibrate the compensating voltage power supply and test the loss of
Outage 14, in Mode 3, NI-36 indication deviated from indication from intermediate range  
      compensating voltage bistable relay driver. On May 17, 2005, during calibration of the
detector NI-35. During interviews with licensed operators, when shutdown banks were  
      compensating voltage, during step 8.2.4.1, the technicians noted that compensating
withdrawn, NI-36 went above 6 E-11 amps and cleared the P-6 interlock while the  
                                          - 63 -                                  Enclosure 2
reactor was subcritical. Indication above 6E-11 normally means the reactor is critical.
The source ranges count rates and NI-35 also increased, but did not indicate criticality.  
Troubleshooting was performed under Work Order 05-272906-000 was performed on  
May 16, 2005. Instrumentation and controls technicians disconnected, cleaned, and  
reconnected NI-36 cables. The NI-36 cables were then disconnected and reconnected  
two more times. Work Order 05-272906-000 was also used to perform STS IC-436,  
Channel Calibration NIS Intermediate Range N-36, Revision 15, test the log current  
amplifier and indicator calibrations, Work Order 05-272906-000 was also used to  
perform STN IC-236, Intermediate Range N36 Compensation Voltage Adjustment,  
Revision 4 to calibrate the compensating voltage power supply and test the loss of  
compensating voltage bistable relay driver. On May 17, 2005, during calibration of the  
compensating voltage, during step 8.2.4.1, the technicians noted that compensating  


voltage was not changing indication permanently, only temporarily. The as-found and
as-left compensating voltage were satisfactory, but the compensating current as-found
and as-left was at 1E-10amps which is one order of magnitude above the 3E-11amps
- 64 -
acceptance criteria. The surveillance was closed stating used only as troubleshooting
tool only. No credit taken. The surveillance test routing sheet noted this as a technical
specification failure. This was then used to generate Work Order 05-272906-000 which
stated that there was a possible problem with the signal cable for NI-32 and the
compensation cable for NI-36 and to rework the cables. The operators had to remove
Enclosure 2
instrument fuses from the NI-36 instrument rack to cause the interlock to clear after the
voltage was not changing indication permanently, only temporarily. The as-found and  
efforts below. During control rod pulls during preparations for criticality, the P-6 interlock
as-left compensating voltage were satisfactory, but the compensating current as-found  
came in with the reactor subcritical. Fuses had to later be pulled and re-inserted to clear
and as-left was at 1E-10amps which is one order of magnitude above the 3E-11amps  
the interlock after NI-36 was worked during this series of work orders.
acceptance criteria. The surveillance was closed stating used only as troubleshooting  
Using Work Order 05-272926-005, the technicians used STS IC-236 to successfully test
tool only. No credit taken. The surveillance test routing sheet noted this as a technical  
the positive and negative 25 Vdc power supplies, the high voltage power supply, the
specification failure. This was then used to generate Work Order 05-272906-000 which  
power above permissive P-6 bistable relay driver, and the reactor trip high level
stated that there was a possible problem with the signal cable for NI-32 and the  
bistable relay driver. However, other than disconnecting cleaning, and reconnecting the
compensation cable for NI-36 and to rework the cables. The operators had to remove  
connectors, no corrective maintenance was performed on cables. The cause of the
instrument fuses from the NI-36 instrument rack to cause the interlock to clear after the  
failure was documented as suspect loose connection. Wolf Creek concluded that after
efforts below. During control rod pulls during preparations for criticality, the P-6 interlock  
the above efforts, that NI-36 indication had been reduced sufficiently to declare it
came in with the reactor subcritical. Fuses had to later be pulled and re-inserted to clear  
operable because it channel checked with NI-35 to within one decade. Reactor startup
the interlock after NI-36 was worked during this series of work orders.  
commenced on May 18, 2005, and concluded Refueling Outage 14.
Using Work Order 05-272926-005, the technicians used STS IC-236 to successfully test  
During a reactor shutdown for Refueling Outage 15 on October 7, 2006, intermediate
the positive and negative 25 Vdc power supplies, the high voltage power supply, the  
range neutron Detector NI-36 did not decrease below 6E -11 amps and energize source
power above permissive P-6 bistable relay driver, and the reactor trip high level  
range detector NI-32. Following NI-36s failure to decrease below the P-6 setpoint,
bistable relay driver. However, other than disconnecting cleaning, and reconnecting the  
reactor operators correctly transitioned to Procedure OFN SB-008, Instrument
connectors, no corrective maintenance was performed on cables. The cause of the  
Malfunctions to manually energize source range detector NI-32. On October 7, 2006,
failure was documented as suspect loose connection. Wolf Creek concluded that after  
Wolf Creek performed STN IC-236 under Work Order 05-274604-000. Detector NI-36
the above efforts, that NI-36 indication had been reduced sufficiently to declare it  
failed STN IC-236, Intermediate Range N36 Compensation Voltage Adjustment,
operable because it channel checked with NI-35 to within one decade. Reactor startup  
Revision 4, because the as-found detector current was outside of the tolerance range at
commenced on May 18, 2005, and concluded Refueling Outage 14.  
9E-11 amps (upper limit is 3E-11 amps) and could not be adjusted to within the
During a reactor shutdown for Refueling Outage 15 on October 7, 2006, intermediate  
tolerance. As-found compensating voltage was within the allowable range.
range neutron Detector NI-36 did not decrease below 6E -11 amps and energize source  
Wolf Creek then replaced the jacks for the triaxial connector using Work
range detector NI-32. Following NI-36s failure to decrease below the P-6 setpoint,  
Order 05-272987-000. Work Order 05-272987-000 stated that the connector was found
reactor operators correctly transitioned to Procedure OFN SB-008, Instrument  
failed but did not state what acceptance criteria it did not meet. Work
Malfunctions to manually energize source range detector NI-32. On October 7, 2006,  
Order 05-272987-000 stated that the cause of the failure was suspect failed connector.
Wolf Creek performed STN IC-236 under Work Order 05-274604-000. Detector NI-36  
Also, Work Order 05-272987-000 took measurements of the compensation voltage cable
failed STN IC-236, Intermediate Range N36 Compensation Voltage Adjustment,  
insulation resistance testing, but stated no acceptance criteria. Work Order 05-272987-
Revision 4, because the as-found detector current was outside of the tolerance range at  
000 the performed surveillance test STS IC-236, Channel Operational Test Nuclear
9E-11 amps (upper limit is 3E-11 amps) and could not be adjusted to within the  
Instrumentation System Intermediate Range N-36 Protection Set II, Revision 17, which
tolerance. As-found compensating voltage was within the allowable range.  
was followed by Work Order 06-289017-000 to perform STN IC-236. On October 17,
Wolf Creek then replaced the jacks for the triaxial connector using Work  
2006, STN IC-236 adjusted the compensating voltage to be more positive. The as-found
Order 05-272987-000. Work Order 05-272987-000 stated that the connector was found  
adjustment of the detector current was less than 1E-11amps, which was outside the
failed but did not state what acceptance criteria it did not meet. Work  
STN IC-236 acceptance criteria. The inspectors noted that the instrument drawer will
Order 05-272987-000 stated that the cause of the failure was suspect failed connector.
not allow detector current to decrease below 1E-11 amps due to a designed idling
Also, Work Order 05-272987-000 took measurements of the compensation voltage cable  
current at 1E-11 amps. As-left current was 1E-11 amps. Later in the outage, control
insulation resistance testing, but stated no acceptance criteria. Work Order 05-272987-
                                    - 64 -                                    Enclosure 2
000 the performed surveillance test STS IC-236, Channel Operational Test Nuclear  
Instrumentation System Intermediate Range N-36 Protection Set II, Revision 17, which  
was followed by Work Order 06-289017-000 to perform STN IC-236. On October 17,  
2006, STN IC-236 adjusted the compensating voltage to be more positive. The as-found  
adjustment of the detector current was less than 1E-11amps, which was outside the  
STN IC-236 acceptance criteria. The inspectors noted that the instrument drawer will  
not allow detector current to decrease below 1E-11 amps due to a designed idling  
current at 1E-11 amps. As-left current was 1E-11 amps. Later in the outage, control  


room operators requested that instrumentation and control workers adjust NI-36
because its output was not tracking with the other intermediate range detector, NI-35.
On November 9, 2006, STN IC-236 was performed again. During this test,
- 65 -
compensation current was unable to be adjusted below 3E-11 amps. The as-found
value was 7E-11 amps and the as-left value was 6E-11 amps. The 6E-11 amp current
was outside the allowable limit, but the surveillance procedure was completed with a
deficiency stating no credit taken. The surveillance cover sheet said that NI-36 was
reading within an order of magnitude of NI-35. The control room logs stated the same.
Enclosure 2
Work Order 06-290208-000 was generated to replace the detector during the Refueling
room operators requested that instrumentation and control workers adjust NI-36  
Outage 16.
because its output was not tracking with the other intermediate range detector, NI-35.  
On March 17, 2008, Wolf Creek tripped from 100 percent power and NI-36 automatically
On November 9, 2006, STN IC-236 was performed again. During this test,  
energized source range detector NI-32. The inspectors checked plant computer data
compensation current was unable to be adjusted below 3E-11 amps. The as-found  
and found that the source range instrument energized at 5E-11 amps which is below the
value was 7E-11 amps and the as-left value was 6E-11 amps. The 6E-11 amp current  
acceptance criteria of greater than 6 E-11amps (P-6 setpoint). The detector was
was outside the allowable limit, but the surveillance procedure was completed with a  
subsequently replaced during Refueling Outage 16.
deficiency stating no credit taken. The surveillance cover sheet said that NI-36 was  
The need to transition to Procedure EMG FR-S2, Response to Loss of Core Shutdown,
reading within an order of magnitude of NI-35. The control room logs stated the same.
was not previously identified in a condition report, operator work around, or operator
Work Order 06-290208-000 was generated to replace the detector during the Refueling  
burden. The inspectors found no other evaluation of the detectors behavior before Wolf
Outage 16.  
Creek ascended to Mode 2 in Refueling Outages 14 and 15. The inspectors found that
On March 17, 2008, Wolf Creek tripped from 100 percent power and NI-36 automatically  
the connector cleaning in Refueling Outage 14 and the jack replacement in Refueling
energized source range detector NI-32. The inspectors checked plant computer data  
Outage 15 were not likely to correct the problem found in STN IC-236. The inspectors
and found that the source range instrument energized at 5E-11 amps which is below the  
concluded that the STN IC-236 surveillances in Refueling Outage 14 and Refueling
acceptance criteria of greater than 6 E-11amps (P-6 setpoint). The detector was  
Outage 15 had not met the acceptance criteria and that startup should not have
subsequently replaced during Refueling Outage 16.  
continued until the nuclear instrument issue was resolved. Wolf Creek did not identify
The need to transition to Procedure EMG FR-S2, Response to Loss of Core Shutdown,  
the issue as a technical specification violation. Although work orders were planned in
was not previously identified in a condition report, operator work around, or operator  
Refueling Outage 14 to replace NI-36, all were closed without action. The inspectors
burden. The inspectors found no other evaluation of the detectors behavior before Wolf  
found that NI-36 was conditioned through troubleshooting until it could pass its one
Creek ascended to Mode 2 in Refueling Outages 14 and 15. The inspectors found that  
decade channel check. Other testing performed by Wolf Creek only impacted the
the connector cleaning in Refueling Outage 14 and the jack replacement in Refueling  
instrument drawer in the control room, while the problem was related to the detector
Outage 15 were not likely to correct the problem found in STN IC-236. The inspectors  
itself. Condition Report 2006-003187 found that the problems with compensating
concluded that the STN IC-236 surveillances in Refueling Outage 14 and Refueling  
voltage could not be determined, but concluded that it was not necessary for operability
Outage 15 had not met the acceptance criteria and that startup should not have  
because the system had no risk significance. The inspectors determined that the
continued until the nuclear instrument issue was resolved. Wolf Creek did not identify  
compensation current is critical to the operation of the detectors because the design of
the issue as a technical specification violation. Although work orders were planned in  
the compensated ion chamber is to allow the instrument drawer to sum currents in
Refueling Outage 14 to replace NI-36, all were closed without action. The inspectors  
opposing directions to discriminate neutrons from gamma. The condition report also
found that NI-36 was conditioned through troubleshooting until it could pass its one  
identified that the P-6 interlock may not work correctly, but no action was taken.
decade channel check. Other testing performed by Wolf Creek only impacted the  
The inspectors reviewed Wolf Creek Technical Specification 3.3.1, Function 18.a,
instrument drawer in the control room, while the problem was related to the detector  
Intermediate Range Flux, P-6 [interlock], and its bases statement. The bases state
itself. Condition Report 2006-003187 found that the problems with compensating  
that Function 18.a ensures that, on decreasing power, the P-6 interlock automatically
voltage could not be determined, but concluded that it was not necessary for operability  
energizes nuclear instrumentation source range detectors and enables the source range
because the system had no risk significance. The inspectors determined that the  
neutron flux reactor trip. During reactor trip, the function is required as reactor power
compensation current is critical to the operation of the detectors because the design of  
decreases to energize the source range detectors and the source range reactor trips.
the compensated ion chamber is to allow the instrument drawer to sum currents in  
The inspectors found that Wolf Creeks bases are consistent with the NUREG-1431,
opposing directions to discriminate neutrons from gamma. The condition report also  
Standard Technical Specifications Westinghouse Plants, Revision 3.0.
identified that the P-6 interlock may not work correctly, but no action was taken.  
                                    - 65 -                                    Enclosure 2
The inspectors reviewed Wolf Creek Technical Specification 3.3.1, Function 18.a,  
Intermediate Range Flux, P-6 [interlock], and its bases statement. The bases state  
that Function 18.a ensures that, on decreasing power, the P-6 interlock automatically  
energizes nuclear instrumentation source range detectors and enables the source range  
neutron flux reactor trip. During reactor trip, the function is required as reactor power  
decreases to energize the source range detectors and the source range reactor trips.
The inspectors found that Wolf Creeks bases are consistent with the NUREG-1431,  
Standard Technical Specifications Westinghouse Plants, Revision 3.0.  


    Analysis. The inspectors determined that the failure to ensure that the P-6 interlock was
    operable per the technical specification as defined in the bases was a performance
    deficiency. The finding was more than minor because it was associated with the
- 66 -
    configuration control (reactivity control) attribute of the Barrier Integrity Cornerstone, and
    it affected the cornerstone objective to provide reasonable assurance that physical
    design barriers (fuel cladding, reactor coolant system, and containment) protect the
    public from radionuclide releases caused by accidents or events. The inspectors
    evaluated the significance of this finding under the Mitigating Systems Cornerstone
Enclosure 2
    using Phase 1 of Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and
Analysis. The inspectors determined that the failure to ensure that the P-6 interlock was  
    Characterization of Findings, and determined that the finding screened to Green
operable per the technical specification as defined in the bases was a performance  
    because the P-6 interlock only affected the fuel barrier. This finding was not assigned a
deficiency. The finding was more than minor because it was associated with the  
    crosscutting aspect because the cause was not representative of current performance.
configuration control (reactivity control) attribute of the Barrier Integrity Cornerstone, and  
    Enforcement. Wolf Creek Technical Specification, Table 3.3.1-1, Function 18.a,
it affected the cornerstone objective to provide reasonable assurance that physical  
    requires, in part, that when intermediate range instrument measured neutron flux
design barriers (fuel cladding, reactor coolant system, and containment) protect the  
    decreases below the allowable value of greater than or equal to 6 E-11 amps that the
public from radionuclide releases caused by accidents or events. The inspectors  
    source range instruments be energized and enable the source range reactor trip signal.
evaluated the significance of this finding under the Mitigating Systems Cornerstone  
    Technical Specification, Table 3.3.1-1, Function 4, requires the intermediate range
using Phase 1 of Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and  
    detectors to be operable at low power in Modes 1 and 2. These functions are required
Characterization of Findings, and determined that the finding screened to Green  
    on reactor trip. Contrary to the above, from May 17, 2005, to March 17, 2008,
because the P-6 interlock only affected the fuel barrier. This finding was not assigned a  
    intermediate range detector NI-36 was inoperable because its output did not decrease
crosscutting aspect because the cause was not representative of current performance.  
    below the P-6 setpoint when the reactor tripped and failed to energize source range
Enforcement. Wolf Creek Technical Specification, Table 3.3.1-1, Function 18.a,  
    instrument NI-32 and the source range reactor trip. Because this violation was
requires, in part, that when intermediate range instrument measured neutron flux  
    determined to be of very low safety significance and was placed in the corrective action
decreases below the allowable value of greater than or equal to 6 E-11 amps that the  
    program as Condition Report 00022450, this violation is being treated as a noncited
source range instruments be energized and enable the source range reactor trip signal.
    violation in accordance with Section VI.A.1 of the Enforcement Policy: NCV
Technical Specification, Table 3.3.1-1, Function 4, requires the intermediate range  
    05000482/2009005-14, Failure to Identify Inoperable P-6 Interlock and Intermediate
detectors to be operable at low power in Modes 1 and 2. These functions are required  
    Range Detector.
on reactor trip. Contrary to the above, from May 17, 2005, to March 17, 2008,  
4OA3 Event Follow-up (71153)
intermediate range detector NI-36 was inoperable because its output did not decrease  
.1   Response to Notice of Unusual Event
below the P-6 setpoint when the reactor tripped and failed to energize source range  
    On October 22, 2009, Emergency Diesel Generator B was out of service for planned
instrument NI-32 and the source range reactor trip. Because this violation was  
    maintenance. At 12:06 p.m., the Wolf Creek control room received trouble annunciators
determined to be of very low safety significance and was placed in the corrective action  
    for Emergency Diesel Generator A. The speed sensor failed high which would cause
program as Condition Report 00022450, this violation is being treated as a noncited  
    any diesel start to fail. This stopped the jacket water keep warm pump, and prevented
violation in accordance with Section VI.A.1 of the Enforcement Policy: NCV  
    air start system solenoids from starting the engine. Since the engine was in standby, low
05000482/2009005-14, Failure to Identify Inoperable P-6 Interlock and Intermediate  
    lube oil pressure also would have prevented the engine from starting. Wolf Creek
Range Detector.  
    initiated troubleshooting and repair. At 5:39 p.m., Wolf Creek declared an Unusual Event
4OA3 Event Follow-up (71153)  
    under Emergency Action Level (EAL) 6/AC5 for loss of both diesels with the reactor
.1  
    defueled. At 5:45 p.m., Wolf Creek made notification to state and local governments of
Response to Notice of Unusual Event  
    the Notice of Unusual Event. At 7:14 p.m., Wolf Creek notified the NRC Operations
On October 22, 2009, Emergency Diesel Generator B was out of service for planned  
    Officer that the power supply had excessive voltage ripple which caused the speed
maintenance. At 12:06 p.m., the Wolf Creek control room received trouble annunciators  
    sensors failure. The speed switch and its power supply were replaced. The inspectors
for Emergency Diesel Generator A. The speed sensor failed high which would cause  
    observed control room activities, repair activities, and post-maintenance testing of
any diesel start to fail. This stopped the jacket water keep warm pump, and prevented  
    repairs. On October 23, 2009, at 7:38 a.m., Emergency Diesel Generator A was
air start system solenoids from starting the engine. Since the engine was in standby, low  
    restored to operable status and the unusual event was terminated.
lube oil pressure also would have prevented the engine from starting. Wolf Creek  
                                          - 66 -                                      Enclosure 2
initiated troubleshooting and repair. At 5:39 p.m., Wolf Creek declared an Unusual Event  
under Emergency Action Level (EAL) 6/AC5 for loss of both diesels with the reactor  
defueled. At 5:45 p.m., Wolf Creek made notification to state and local governments of  
the Notice of Unusual Event. At 7:14 p.m., Wolf Creek notified the NRC Operations  
Officer that the power supply had excessive voltage ripple which caused the speed  
sensors failure. The speed switch and its power supply were replaced. The inspectors  
observed control room activities, repair activities, and post-maintenance testing of  
repairs. On October 23, 2009, at 7:38 a.m., Emergency Diesel Generator A was  
restored to operable status and the unusual event was terminated.  


  b. Findings
      One violation of very low safety significance (Green) is described in Section 4OA7 of this
      report.
- 67 -
.2   Licensee Event Report Review
  a. Inspection Scope
      The inspectors reviewed potentially reportable events under Inspection
      Procedure IP 71153. Inspectors also utilized NUREG 1022, Event Reporting Guidelines
      10 CFR 50.72 and 50.73, Revision 2.
Enclosure 2
  b. Findings
b.  
      Introduction. The inspectors identified a Severity Level IV noncited violation of
Findings  
      10 CFR 50.73, in which the licensee failed to submit licensee event reports within 60
One violation of very low safety significance (Green) is described in Section 4OA7 of this  
      days following discovery of events or conditions meeting the reportability criteria.
report.
      Description. The licensee submitted Licensee Event Report LER 2009-009-00 under
.2
      10 CFR 50.73(a)(2)(i)(B) for an operation prohibited by technical specifications. The
Licensee Event Report Review
      inspectors determined this event report was not submitted within the 60 days allowed by
a.  
      10 CFR 50.73. The inspectors identified that other reporting requirements of 50.73 also
Inspection Scope  
      applied but were not included in the licensee event report.
The inspectors reviewed potentially reportable events under Inspection  
      In the event on August 22, 2009, Wolf Creek disabled both trains of the P-4 interlock for
Procedure IP 71153. Inspectors also utilized NUREG 1022, Event Reporting Guidelines  
      planned maintenance. Specifically, the feedwater isolation signal that is generated by
10 CFR 50.72 and 50.73, Revision 2.  
      P-4 (reactor trip coincident with low Tave) was taken out of service for control rod drive
b.  
      motor-generator set testing. This allowed reactor trip breaker cycling without isolation of
Findings  
      main feedwater. The P-4 interlock was required by Technical Specification 3.3.2 function
Introduction. The inspectors identified a Severity Level IV noncited violation of  
      8.a. This function is discussed in USAR Section 7.3.8, NSSS Engineered Safety
10 CFR 50.73, in which the licensee failed to submit licensee event reports within 60  
      Feature Actuation System. which describes the function of a main feedwater isolation as
days following discovery of events or conditions meeting the reportability criteria.  
      to prevent or mitigate the effect of an excessive cooldown. Wolf Creek technical
Description. The licensee submitted Licensee Event Report LER 2009-009-00 under  
      specification Bases also state that one or more functions may backup other engineered
10 CFR 50.73(a)(2)(i)(B) for an operation prohibited by technical specifications. The  
      safety feature actuation signal functions credited in Chapter 15 of the USAR.
inspectors determined this event report was not submitted within the 60 days allowed by  
      Licensee Event Report 2009-009-00 reported a condition prohibited by technical
10 CFR 50.73. The inspectors identified that other reporting requirements of 50.73 also  
      specifications under a(2)(i)(B) and correctly described that the P-4 interlock was not
applied but were not included in the licensee event report.  
      credited in accident analysis. The licensee did not report the event under reporting
In the event on August 22, 2009, Wolf Creek disabled both trains of the P-4 interlock for  
      criteria 50.73(a)(2)(v). The engineered safety features actuation signal system has other
planned maintenance. Specifically, the feedwater isolation signal that is generated by  
      signals that cause feedwater isolations that are used in Chapter 15 of the USAR.
P-4 (reactor trip coincident with low Tave) was taken out of service for control rod drive  
      The inspectors consulted NUREG 1022, Event Reporting Guidelines 10 CFR 50.72
motor-generator set testing. This allowed reactor trip breaker cycling without isolation of  
      and 50.73, Revision 2. NUREG 1022, Section 3.2.7, reportability under 50.73(a)(2)(v),
main feedwater. The P-4 interlock was required by Technical Specification 3.3.2 function  
      specified that inoperable systems required by the technical specifications are to be
8.a. This function is discussed in USAR Section 7.3.8, NSSS Engineered Safety  
      reported, even if there are other diverse, operable means of accomplishing the safety
Feature Actuation System. which describes the function of a main feedwater isolation as  
      function. The inspectors found that Wolf Creek was not correct in concluding that the
to prevent or mitigate the effect of an excessive cooldown. Wolf Creek technical  
      50.73(a)(2)(v)(A) through (D) only applied to the accident analysis contained in
specification Bases also state that one or more functions may backup other engineered  
      Chapter 15 of the USAR. The inspectors consulted with the NRC Office of Nuclear
safety feature actuation signal functions credited in Chapter 15 of the USAR.  
                                          - 67 -                                  Enclosure 2
Licensee Event Report 2009-009-00 reported a condition prohibited by technical  
specifications under a(2)(i)(B) and correctly described that the P-4 interlock was not  
credited in accident analysis. The licensee did not report the event under reporting  
criteria 50.73(a)(2)(v). The engineered safety features actuation signal system has other  
signals that cause feedwater isolations that are used in Chapter 15 of the USAR.  
The inspectors consulted NUREG 1022, Event Reporting Guidelines 10 CFR 50.72  
and 50.73, Revision 2. NUREG 1022, Section 3.2.7, reportability under 50.73(a)(2)(v),  
specified that inoperable systems required by the technical specifications are to be  
reported, even if there are other diverse, operable means of accomplishing the safety  
function. The inspectors found that Wolf Creek was not correct in concluding that the  
50.73(a)(2)(v)(A) through (D) only applied to the accident analysis contained in  
Chapter 15 of the USAR. The inspectors consulted with the NRC Office of Nuclear  


      Reactor Regulation, who agreed with the inspectors application of the rule and
      NUREG 1022. The untimely licensee event report was entered into the corrective action
      program as Condition Report 22781.
- 68 -
      Analysis. The failure to submit a timely and complete licensee event report was a
      performance deficiency. The inspectors reviewed this issue in accordance with
      Inspection Manual Chapter 0612 and the NRC Enforcement Manual. Through this
      review, the inspectors determined that traditional enforcement was applicable to this
      issue because the NRC's regulatory ability was affected. Specifically, the NRC relies on
Enclosure 2
      the licensee to identify and report conditions or events meeting the criteria specified in
Reactor Regulation, who agreed with the inspectors application of the rule and  
      regulations in order to perform its regulatory function, and when this is not done, the
NUREG 1022. The untimely licensee event report was entered into the corrective action  
      regulatory function is impacted. The inspectors determined that this finding was not
program as Condition Report 22781.  
      suitable for evaluation using the significance determination process, and as such, was
Analysis. The failure to submit a timely and complete licensee event report was a  
      evaluated in accordance with the NRC Enforcement Policy. The finding was reviewed
performance deficiency. The inspectors reviewed this issue in accordance with  
      by NRC management, and because the violation was determined to be of very low
Inspection Manual Chapter 0612 and the NRC Enforcement Manual. Through this  
      safety significance, was not repetitive or willful, and was entered into the corrective
review, the inspectors determined that traditional enforcement was applicable to this  
      action program, this violation is being treated as a Severity Level IV noncited violation
issue because the NRC's regulatory ability was affected. Specifically, the NRC relies on  
      consistent with the NRC Enforcement Policy. This finding was determined to have a
the licensee to identify and report conditions or events meeting the criteria specified in  
      crosscutting aspect in the area of problem identification and resolution associated with
regulations in order to perform its regulatory function, and when this is not done, the  
      the corrective action program in that the licensee failed to appropriately and thoroughly
regulatory function is impacted. The inspectors determined that this finding was not  
      evaluate for reportability aspects all factors and time frames associated with the
suitable for evaluation using the significance determination process, and as such, was  
      inoperability of the engineered safety features actuation system [P.1(c)].
evaluated in accordance with the NRC Enforcement Policy. The finding was reviewed  
      Enforcement. Title 10 CFR 50.73(a)(1) requires, in part, that licensees shall submit a
by NRC management, and because the violation was determined to be of very low  
      licensee event report for any event of the type described in this paragraph within 60
safety significance, was not repetitive or willful, and was entered into the corrective  
      days after the discovery of the event. Title 10 CFR 50.73(a)(2)(v) requires, in part, that
action program, this violation is being treated as a Severity Level IV noncited violation  
      events or conditions that could have prevented the fulfillment of the safety function of
consistent with the NRC Enforcement Policy. This finding was determined to have a  
      structures or systems that are needed to shutdown the reactor and maintain it in a safe
crosscutting aspect in the area of problem identification and resolution associated with  
      shutdown condition, remove residual heat, control the release of radioactive material, or
the corrective action program in that the licensee failed to appropriately and thoroughly  
      mitigate the consequences of an accident. Contrary to the above, on October 23, 2009,
evaluate for reportability aspects all factors and time frames associated with the  
      Wolf Creek failed to submit a licensee event report within 60 days for removing the P-4
inoperability of the engineered safety features actuation system [P.1(c)].  
      interlock from service, and failed to identify that the condition could have prevented the
      fulfillment of the safety function of structures or systems that are needed to mitigate the
Enforcement. Title 10 CFR 50.73(a)(1) requires, in part, that licensees shall submit a  
      consequences of an accident. In accordance with the NRC's Enforcement Policy, the
licensee event report for any event of the type described in this paragraph within 60  
      finding was reviewed by NRC management and because the violation was of very low
days after the discovery of the event. Title 10 CFR 50.73(a)(2)(v) requires, in part, that  
      safety significance, was not repetitive or willful, and was entered into the corrective
events or conditions that could have prevented the fulfillment of the safety function of  
      action program, this violation is being treated as a Severity Level IV noncited violation,
structures or systems that are needed to shutdown the reactor and maintain it in a safe  
      consistent with the NRC Enforcement Policy: NCV 05000482/2009005-15, Failure to
shutdown condition, remove residual heat, control the release of radioactive material, or  
      Report a Condition that Could Have Prevented Fulfillment of a Safety Function.
mitigate the consequences of an accident. Contrary to the above, on October 23, 2009,  
4OA5 Other Activities
Wolf Creek failed to submit a licensee event report within 60 days for removing the P-4  
.1   Quarterly Resident Inspector Observations of Security Personnel and Activities
interlock from service, and failed to identify that the condition could have prevented the  
  a. Inspection Scope
fulfillment of the safety function of structures or systems that are needed to mitigate the  
      During the inspection period, the inspectors performed observations of security force
consequences of an accident. In accordance with the NRC's Enforcement Policy, the  
      personnel and activities to ensure that the activities were consistent with Wolf Creek
finding was reviewed by NRC management and because the violation was of very low  
                                            - 68 -                                  Enclosure 2
safety significance, was not repetitive or willful, and was entered into the corrective  
action program, this violation is being treated as a Severity Level IV noncited violation,  
consistent with the NRC Enforcement Policy: NCV 05000482/2009005-15, Failure to  
Report a Condition that Could Have Prevented Fulfillment of a Safety Function.  
4OA5 Other Activities
.1  
Quarterly Resident Inspector Observations of Security Personnel and Activities  
a.  
Inspection Scope  
During the inspection period, the inspectors performed observations of security force  
personnel and activities to ensure that the activities were consistent with Wolf Creek  


        security procedures and regulatory requirements relating to nuclear plant security.
        These observations took place during both normal and off-normal plant working hours.
        These quarterly resident inspector observations of security force personnel and activities
- 69 -
        did not constitute any additional inspection samples. Rather, they were considered an
        integral part of the inspectors normal plant status review and inspection activities.
  b.   Findings
        No findings of significance were identified.
.2     Temporary Instruction 2515-172, Reactor Coolant System Dissimilar Metal Butt Welds
Enclosure 2
  a.   Inspection Scope:
security procedures and regulatory requirements relating to nuclear plant security.
        Portions of Temporary Instruction 2515/172, Reactor Coolant System Dissimilar Metal
These observations took place during both normal and off-normal plant working hours.  
        Butt Welds, were performed at Wolf Creek during Refueling Outage 17. Specific
These quarterly resident inspector observations of security force personnel and activities  
        documents reviewed during this inspection are listed in the attachment. This unit has
did not constitute any additional inspection samples. Rather, they were considered an  
        the following dissimilar metal butt welds.
integral part of the inspectors normal plant status review and inspection activities.  
      COMPONENT ID           DESCRIPTION         MRP-139       BASELINE           COMMENT
b.  
                                                CATEGORY            EXAM
Findings  
    RV-301-121-A           Loop 1 Outlet             D            April 2005        Next exam:
No findings of significance were identified.  
                            Nozzle to Safe-
.2  
                            end weld                                 RF14           October 2009
Temporary Instruction 2515-172, Reactor Coolant System Dissimilar Metal Butt Welds  
                                                                                        RF17
    RV-301-121-B           Loop 2 Outlet             D            April 2005        Next exam:
a.
                            Nozzle to Safe-
Inspection Scope:  
                            end weld                                 RF14           October 2009
                                                                                        RF17
Portions of Temporary Instruction 2515/172, Reactor Coolant System Dissimilar Metal  
    RV-301-121-C           Loop 3 Outlet             D            April 2005        Next exam:
Butt Welds, were performed at Wolf Creek during Refueling Outage 17. Specific  
                            Nozzle to Safe-
documents reviewed during this inspection are listed in the attachment. This unit has  
                            end weld                                 RF14           October 2009
the following dissimilar metal butt welds.
                                                                                        RF17
    RV-301-121-D           Loop 4 Outlet             D            April 2005        Next exam:
COMPONENT ID  
                            Nozzle to Safe-
DESCRIPTION
                            end weld                                 RF14           October 2009
MRP-139  
                                                                                        RF17
CATEGORY
    RV-302-121-A           Loop 1 Inlet             E            April 2005        Next exam:
BASELINE  
                            Nozzle to Safe-
EXAM  
                            end weld                                 RF14         April 2011 RF18
COMMENT
    RV-302-121-B           Loop 2 Inlet             E           April 2005       Next exam:
RV-301-121-A  
                            Nozzle to Safe-
Loop 1 Outlet  
                                            - 69 -                                  Enclosure 2
Nozzle to Safe-
end weld  
D
April 2005
RF14  
Next exam:
October 2009  
RF17  
RV-301-121-B  
Loop 2 Outlet  
Nozzle to Safe-
end weld  
D
April 2005
RF14  
Next exam:
October 2009  
RF17  
RV-301-121-C  
Loop 3 Outlet  
Nozzle to Safe-
end weld  
D
April 2005
RF14  
Next exam:
October 2009  
RF17  
RV-301-121-D  
Loop 4 Outlet  
Nozzle to Safe-
end weld  
D
April 2005
RF14  
Next exam:
October 2009  
RF17  
RV-302-121-A  
Loop 1 Inlet  
Nozzle to Safe-
end weld  
E
April 2005
RF14  
Next exam:
April 2011 RF18  
RV-302-121-B  
Loop 2 Inlet  
Nozzle to Safe-
E  
April 2005  
Next exam:  


  COMPONENT ID           DESCRIPTION           MRP-139       BASELINE           COMMENT
   
                                            CATEGORY            EXAM
                      end weld                                 RF14         April 2011 RF18
- 70 -
RV-302-121-C           Loop 3 Inlet             E            April 2005        Next exam:
                      Nozzle to Safe-
                      end weld                                 RF14         April 2011 RF18
RV-302-121-D           Loop 4 Inlet             E            April 2005        Next exam:
                      Nozzle to Safe-
Enclosure 2
                      end weld                                 RF14         April 2011 RF18
COMPONENT ID  
TBB03-1-W /           Pressurizer surge       D/F         October 2006           Note 1
DESCRIPTION
                      nozzle to safe-                           RF15
MRP-139  
MW7090-WOL-DM         end weld
CATEGORY
TBB03-2-W /            Pressurizer spray        D/B         October 2006           Note 1
BASELINE  
                      nozzle to safe-                          RF15
EXAM  
MW7089-WOL-DM          end weld
COMMENT
TBB03-3-A-W /         Pressurizer             D/B          October 2006          Note 1
end weld  
                      safety nozzle A to                       RF15
RF14  
MW7086-WOL-DM          safe-end weld
April 2011 RF18  
TBB03-3-B-W /         Pressurizer             D/B          October 2006          Note 1
RV-302-121-C  
                      safety nozzle B to                       RF15
Loop 3 Inlet  
MW7087-WOL-DM          Safe-end weld
Nozzle to Safe-
TBB03-3-C-W /         Pressurizer             D/F          October 2006          Note 1
end weld  
                      safety nozzle C                           RF15
E
MW7088-WOL-DM          to safe-end weld
April 2005
TBB03-4-W /            Pressurizer relief      D/F         October 2006           Note 1
RF14  
                      nozzle to safe-                           RF15
Next exam:
MW7085-WOL-DM         end weld
April 2011 RF18  
  Note 1: The pressurizer dissimilar metal butt-welds had full structural weld overlay
RV-302-121-D  
  applied in Refueling Outage 15. The first Component ID was the designation prior to
Loop 4 Inlet  
  overlay, the latter Component ID is the current weld designation (after overlay).
Nozzle to Safe-
  Likewise, the first MRP-139 category was the designation prior to baseline exam and
end weld  
  overlay, and the latter is the current designation (after overlay). Note that these
E
  locations are now examined in accordance with approved alternative of relief
April 2005
  Request I3R-05.
RF14  
                                        - 70 -                                  Enclosure 2
Next exam:
April 2011 RF18  
TBB03-1-W /  
MW7090-WOL-DM
Pressurizer surge  
nozzle to safe-
end weld
D / F  
October 2006  
RF15
Note 1  
TBB03-2-W /
MW7089-WOL-DM  
Pressurizer spray
nozzle to safe-
end weld  
D / B  
October 2006  
RF15  
Note 1
TBB03-3-A-W /  
MW7086-WOL-DM
Pressurizer  
safety nozzle A to  
safe-end weld  
D / B
October 2006
RF15
Note 1
TBB03-3-B-W /  
MW7087-WOL-DM
Pressurizer  
safety nozzle B to  
Safe-end weld  
D / B
October 2006
RF15
Note 1
TBB03-3-C-W /  
MW7088-WOL-DM
Pressurizer  
safety nozzle C  
to safe-end weld  
D / F  
October 2006  
RF15
Note 1  
TBB03-4-W /
MW7085-WOL-DM  
Pressurizer relief
nozzle to safe-
end weld  
D / F
October 2006
RF15
Note 1
Note 1: The pressurizer dissimilar metal butt-welds had full structural weld overlay  
applied in Refueling Outage 15. The first Component ID was the designation prior to  
overlay, the latter Component ID is the current weld designation (after overlay).
Likewise, the first MRP-139 category was the designation prior to baseline exam and  
overlay, and the latter is the current designation (after overlay). Note that these  
locations are now examined in accordance with approved alternative of relief  
Request I3R-05.  


03.01 Licensees Implementation of the MRP-139 Baseline Inspections
  a. MRP-139 baseline inspections:
      The inspectors reviewed records nondestructive examination activities associated with
- 71 -
      the licensees hot leg inspection effort. The baseline inspections of the pressurizer
      dissimilar metal butt welds were completed during the spring 2008 Refueling Outage 16.
  b. At the present time, the licensee is not planning to take any deviations from the baseline
      inspection requirements of MRP-139, and all other applicable dissimilar metal butt welds
      are scheduled in accordance with MRP-139 guidelines.
Enclosure 2
03.02 Volumetric Examinations
03.01 Licensees Implementation of the MRP-139 Baseline Inspections  
  a. The inspectors reviewed the ultrasonic examination records of the four unmitigated
      reactor hot leg nozzles and piping. The inspectors concluded that the ultrasonic
a.  
      examination for these welds was done in accordance with ASME Code, Section XI,
MRP-139 baseline inspections:  
      Supplement VIII, Performance Demonstration Initiative requirements regarding
      personnel, procedures, and equipment qualifications. No relevant conditions were
The inspectors reviewed records nondestructive examination activities associated with  
      identified during these examinations.
the licensees hot leg inspection effort. The baseline inspections of the pressurizer  
  b. The inspectors reviewed the nondestructive evaluations performed on the four reactor
dissimilar metal butt welds were completed during the spring 2008 Refueling Outage 16.  
      hot leg nozzles and piping. Inspection coverage met the requirements of MRP-139 and
      no relevant conditions were identified.
b.  
  c.   The certification records of examination personnel were reviewed for those personnel
At the present time, the licensee is not planning to take any deviations from the baseline  
      that performed the examinations of the inspected nozzles. All personnel records
inspection requirements of MRP-139, and all other applicable dissimilar metal butt welds  
      showed that they were qualified under the EPRI Performance Demonstration Initiative.
are scheduled in accordance with MRP-139 guidelines.
  d. No deficiencies were identified during the nondestructive evaluations.
03.03 Weld Overlays.
03.02 Volumetric Examinations  
      The licensee performed all weld overlays during the previous outage (RF 15).
03.04 Mechanical Stress Improvement
a.  
      The licensee did not employ a mechanical stress improvement process this outage.
The inspectors reviewed the ultrasonic examination records of the four unmitigated  
03.05 Inservice inspection program
reactor hot leg nozzles and piping. The inspectors concluded that the ultrasonic  
  a. Inspection Scope:
examination for these welds was done in accordance with ASME Code, Section XI,  
      The licensees MRP-139 program is part of their Alloy 600 program and future
Supplement VIII, Performance Demonstration Initiative requirements regarding  
      inspections are in accordance with the MRP-139 requirements.
personnel, procedures, and equipment qualifications. No relevant conditions were  
                                          - 71 -                                  Enclosure 2
identified during these examinations.
b.  
The inspectors reviewed the nondestructive evaluations performed on the four reactor  
hot leg nozzles and piping. Inspection coverage met the requirements of MRP-139 and  
no relevant conditions were identified.  
c.  
The certification records of examination personnel were reviewed for those personnel  
that performed the examinations of the inspected nozzles. All personnel records  
showed that they were qualified under the EPRI Performance Demonstration Initiative.  
d.  
No deficiencies were identified during the nondestructive evaluations.  
03.03 Weld Overlays.  
The licensee performed all weld overlays during the previous outage (RF 15).  
03.04 Mechanical Stress Improvement  
The licensee did not employ a mechanical stress improvement process this outage.  
03.05 Inservice inspection program  
a.  
Inspection Scope:  
The licensees MRP-139 program is part of their Alloy 600 program and future  
inspections are in accordance with the MRP-139 requirements.  


  b. Findings
      No findings of significance were identified.
.3   (Closed) Unresolved Item 05000482/2008010-04: Operator Actions May Create the
- 72 -
      Potential for Secondary Fires
      Introduction. The inspectors identified a Green non-cited violation of License
      Condition 2.C.(5), Fire Protection, for the failure to implement and maintain the
      approved fire protection program. Specifically, the licensee prescribed mitigating actions
      in response to certain fire scenarios that would result in a loss of circuit breaker
Enclosure 2
      coordination and could initiate secondary fires in plant locations outside of the initial fire
b.  
      area.
Findings  
      Description. Procedure OFN KC-016, Fire Response, Revision 19, specified operator
      actions to be taken in response to fires outside of the control room. This procedure
No findings of significance were identified.  
      provided the mitigating actions needed to maintain the reactor in hot standby in the
      event of various failures and spurious actuations. The inspectors identified the following
.3  
      13 fire areas where the prescribed mitigating actions would remove electrical circuit
(Closed) Unresolved Item 05000482/2008010-04: Operator Actions May Create the  
      protection (i.e., circuit breaker coordination) for the train affected by the fire and could
Potential for Secondary Fires  
      initiate secondary fires in plant locations outside of the initial fire area:
Introduction. The inspectors identified a Green non-cited violation of License  
      *       Fire Area A-8           Auxiliary Building - 2000 Elevation, General Area
Condition 2.C.(5), Fire Protection, for the failure to implement and maintain the  
      *       Fire Area A-11         Cable Chase (Room 1335)
approved fire protection program. Specifically, the licensee prescribed mitigating actions  
      *       Fire Area A-16         Auxiliary Building - 2026 Elevation, General Area
in response to certain fire scenarios that would result in a loss of circuit breaker  
      *       Fire Area A-17         South Electrical Penetration (Room 1409)
coordination and could initiate secondary fires in plant locations outside of the initial fire  
      *       Fire Area A-18         North Electrical Penetration (Room 1410)
area.  
      *       Fire Area C-18         North Vertical Cable Chase (Room 3419)
Description. Procedure OFN KC-016, Fire Response, Revision 19, specified operator  
      *       Fire Area C-21         Lower Cable Spreading (Room 3501)
actions to be taken in response to fires outside of the control room. This procedure  
      *       Fire Area C-22         Upper Cable Spreading (Room 3801)
provided the mitigating actions needed to maintain the reactor in hot standby in the  
      *       Fire Area C-23         South Vertical Cable Chase (Room 3505)
event of various failures and spurious actuations. The inspectors identified the following  
      *       Fire Area C-24         North Electrical Chase (Room 3504)
13 fire areas where the prescribed mitigating actions would remove electrical circuit  
      *       Fire Area C-30         South Vertical Cable Chase (Room 3617)
protection (i.e., circuit breaker coordination) for the train affected by the fire and could  
      *       Fire Area C-33         South Vertical Cable Chase (Room 3804)
initiate secondary fires in plant locations outside of the initial fire area:  
      *       Fire Area RB           Reactor Building (Containment)
*  
      For these fire areas, the procedure directed the operators to remove power to a
Fire Area A-8  
      power-operated relief valve if a fire caused the power-operated relief valve to spuriously
Auxiliary Building - 2000 Elevation, General Area  
      open and operators could not close its associated block valve. Specifically, the
*  
      procedure directed the operators to open circuit breakers on the associated 125 Vdc
Fire Area A-11  
      power supply. The inspectors noted that the failure of the block valve to close resulted
Cable Chase (Room 1335)  
      from fire damage and not from a spurious operation of the valve.
*  
      The licensee specified this action in order to close the power-operated relief valve and
Fire Area A-16  
      preclude the potential for spurious opening due to inter-cable faults (i.e., cable-to-cable
Auxiliary Building - 2026 Elevation, General Area  
      hot shorts). However, the inspectors determined this action would also remove the
*  
      control power used to operate 4160 Vac and 480 Vac circuit breakers. The removal of
Fire Area A-17  
                                            - 72 -                                    Enclosure 2
South Electrical Penetration (Room 1409)  
*  
Fire Area A-18  
North Electrical Penetration (Room 1410)  
*  
Fire Area C-18  
North Vertical Cable Chase (Room 3419)  
*  
Fire Area C-21  
Lower Cable Spreading (Room 3501)  
*  
Fire Area C-22  
Upper Cable Spreading (Room 3801)  
*  
Fire Area C-23  
South Vertical Cable Chase (Room 3505)  
*  
Fire Area C-24  
North Electrical Chase (Room 3504)  
*  
Fire Area C-30  
South Vertical Cable Chase (Room 3617)  
*  
Fire Area C-33  
South Vertical Cable Chase (Room 3804)  
*  
Fire Area RB  
Reactor Building (Containment)  
For these fire areas, the procedure directed the operators to remove power to a  
power-operated relief valve if a fire caused the power-operated relief valve to spuriously  
open and operators could not close its associated block valve. Specifically, the  
procedure directed the operators to open circuit breakers on the associated 125 Vdc  
power supply. The inspectors noted that the failure of the block valve to close resulted  
from fire damage and not from a spurious operation of the valve.  
The licensee specified this action in order to close the power-operated relief valve and  
preclude the potential for spurious opening due to inter-cable faults (i.e., cable-to-cable  
hot shorts). However, the inspectors determined this action would also remove the  
control power used to operate 4160 Vac and 480 Vac circuit breakers. The removal of  


control power would prevent remote breaker operations and disable the circuit breaker
protective trips for the train affected by the fire.
Removing control power to the circuit breaker results in a loss of its ability to
- 73 -
automatically isolate faults before severe damage occurs. As a result, fire-induced faults
(shorts to ground) in non-essential power cables of the affected 4160 Vac and 480 Vac
supplies may not clear until after tripping an upstream feeder breaker to the supplies,
which would remove power from equipment that was assumed by the safe shutdown
analysis to be unaffected. This action would also prevent breakers from automatically
Enclosure 2
opening during an overload condition and could initiate secondary fires in plant locations
control power would prevent remote breaker operations and disable the circuit breaker  
outside of the initial fire area.
protective trips for the train affected by the fire.  
The safe shutdown analysis assumed that a fire occurred in one fire area at any time.
Removing control power to the circuit breaker results in a loss of its ability to  
The inspectors determined that the mitigating actions taken in response to fires in the
automatically isolate faults before severe damage occurs. As a result, fire-induced faults  
listed fire areas had the potential to initiate secondary fires in other plant locations, which
(shorts to ground) in non-essential power cables of the affected 4160 Vac and 480 Vac  
would invalidate the safe shutdown analysis and could impact the ability to achieve and
supplies may not clear until after tripping an upstream feeder breaker to the supplies,  
maintain safe shutdown.
which would remove power from equipment that was assumed by the safe shutdown  
Analysis. Prescribing mitigating actions in response to certain fire scenarios that would
analysis to be unaffected. This action would also prevent breakers from automatically  
result in a loss of circuit breaker coordination and could initiate secondary fires in plant
opening during an overload condition and could initiate secondary fires in plant locations  
locations outside of the initial fire area was a performance deficiency. The inspectors
outside of the initial fire area.  
determined that this deficiency was more than minor because it was associated with the
The safe shutdown analysis assumed that a fire occurred in one fire area at any time.
Protection Against External Factors attribute of the Initiating Events Cornerstone and
The inspectors determined that the mitigating actions taken in response to fires in the  
adversely affected the cornerstone objective to limit the likelihood of those events that
listed fire areas had the potential to initiate secondary fires in other plant locations, which  
upset plant stability and challenge critical safety functions during shutdown as well as
would invalidate the safe shutdown analysis and could impact the ability to achieve and  
power operations.
maintain safe shutdown.  
The significance of this finding was evaluated using the Significance Determination
Analysis. Prescribing mitigating actions in response to certain fire scenarios that would  
Process in Manual Chapter 0609, Appendix F, Fire Protection Significance
result in a loss of circuit breaker coordination and could initiate secondary fires in plant  
Determination Process, because it affected fire protection defense-in-depth strategies
locations outside of the initial fire area was a performance deficiency. The inspectors  
involving post-fire safe shutdown systems.
determined that this deficiency was more than minor because it was associated with the  
The inspectors associated the finding with the post-fire safe shutdown category since the
Protection Against External Factors attribute of the Initiating Events Cornerstone and  
performance deficiency would remove power from equipment that was assumed by the
adversely affected the cornerstone objective to limit the likelihood of those events that  
safe shutdown analysis to be unaffected and could initiate secondary fires in plant
upset plant stability and challenge critical safety functions during shutdown as well as  
locations outside of the initial fire area. The inspectors assigned the finding a high
power operations.  
degradation rating since the affected circuit breakers would not provide any fire
The significance of this finding was evaluated using the Significance Determination  
protection benefit and would receive no fire protection credit.
Process in Manual Chapter 0609, Appendix F, Fire Protection Significance  
The inspectors performed a Phase 2 evaluation to determine an upper limit for the
Determination Process, because it affected fire protection defense-in-depth strategies  
change in core damage frequency. The inspectors determined eight credible fire
involving post-fire safe shutdown systems.  
scenarios that could result in core damage under certain conservative assumptions. The
The inspectors associated the finding with the post-fire safe shutdown category since the  
pertinent parameters and results of these scenarios are summarized below.
performance deficiency would remove power from equipment that was assumed by the  
Attachment B provides a more detailed discussion of the Phase 2 evaluation.
safe shutdown analysis to be unaffected and could initiate secondary fires in plant  
                                      - 73 -                                    Enclosure 2
locations outside of the initial fire area. The inspectors assigned the finding a high  
degradation rating since the affected circuit breakers would not provide any fire  
protection benefit and would receive no fire protection credit.  
The inspectors performed a Phase 2 evaluation to determine an upper limit for the  
change in core damage frequency. The inspectors determined eight credible fire  
scenarios that could result in core damage under certain conservative assumptions. The  
pertinent parameters and results of these scenarios are summarized below.
Attachment B provides a more detailed discussion of the Phase 2 evaluation.  


                                    Table 1. Phase 2 Evaluation Results
                      Source
                                        Fire       Heat                           Probability
- 74 -
Scenario    Ignition Description                          Severity Probability of
                                      Ignition  Release                            of a Hot   CCDP
Number      Source                                          Factor  Non-Suppression
                                    Frequency      Rate                              Short
                    (Fire Area)
Enclosure 2
                    Relay
Table 1. Phase 2 Evaluation Results  
                    Panel
Scenario
  1      RP-333                      6.00E-5     200 kW     0.9         0.35         0.02     3.78E-7
Number
                    (A-16)
Ignition
                    Relay
Source
                    Panel
Source  
  2      RP-333                      6.00E-5     650 kW     0.1         0.35         0.02     4.20E-8
Description
                    (A-16)
(Fire Area)
                    Security
Fire  
                    Panel
Ignition
  3      SK194B                      6.00E-5     200 kW     0.1         0.35         0.02     4.20E-8
Frequency
                    (A-16)
Heat  
                    600V MCC
Release
  4      NG01B                      6.00E-5     200 kW     0.1         0.44         0.02     5.28E-8
Rate
                    (A-18)
Severity  
          Transient
Factor
  5                C-21             6.26E-6     70 kW     0.9         0.26         0.02     2.93E-8
Probability of  
          Fire
Non-Suppression
          Transient
Probability
  6                C-21             6.26E-6     200 kW     0.1         0.26         0.02     3.26E-9
of a Hot  
          Fire
Short
          Transient
CCDP  
  7                C-22             5.54E-6     70 kW     0.9         1.00         0.02     9.96E-8
1
          Fire
RP-333
          Transient
Relay  
  8                C-22             5.54E-6     200 kW     0.1         1.00         0.02     1.11E-8
Panel  
          Fire
(A-16)
                                                                                      Total     6.58E-7
6.00E-5  
      In each of these scenarios, the conditional core damage probability (CCDP) bounds the
200 kW  
      change in core damage frequency. The inspectors calculated the conditional core
0.9  
      damage probability using the following equation:
0.35  
                      CCDP = FIF x SF x PNon  Suppression x PHot Short
0.02  
      where:          FIF denotes the fire ignition frequency
3.78E-7  
                        SF denotes the severity factor
2
                        PNon  Suppression denotes the non-suppression probability
RP-333
                                                - 74 -                                  Enclosure 2
Relay  
Panel  
(A-16)
6.00E-5  
650 kW  
0.1  
0.35  
0.02  
4.20E-8  
3
SK194B
Security
Panel
(A-16)  
6.00E-5  
200 kW  
0.1  
0.35  
0.02  
4.20E-8  
4
NG01B
600V MCC
(A-18)  
6.00E-5  
200 kW  
0.1  
0.44  
0.02  
5.28E-8  
5
Transient  
Fire
C-21  
6.26E-6  
70 kW  
0.9  
0.26  
0.02  
2.93E-8  
6
Transient  
Fire
C-21  
6.26E-6  
200 kW  
0.1  
0.26  
0.02  
3.26E-9  
7
Transient  
Fire
C-22  
5.54E-6  
70 kW  
0.9  
1.00  
0.02  
9.96E-8  
8
Transient  
Fire
C-22  
5.54E-6  
200 kW  
0.1  
1.00  
0.02  
1.11E-8  
Total  
6.58E-7  
In each of these scenarios, the conditional core damage probability (CCDP) bounds the  
change in core damage frequency. The inspectors calculated the conditional core  
damage probability using the following equation:  
Short
Hot
n
Suppressio
Non
P
x
P
x
SF
x
FIF
CCDP


                  PHot Short denotes the probability of a hot short
=
The sum of the conditional core damage probabilities for each of the fire scenarios
bounded the total change in core damage frequency associated with this performance
where: 
deficiency. Since the change in core damage frequency exceeded1E-7, the inspectors
FIF  denotes the fire ignition frequency  
screened the finding for its potential risk contribution to a large early release frequency.
In accordance with the guidance in NRC Inspection Manual Chapter 0609, Appendix H,
the inspectors determined this finding did not involve a significant increase in the risk of
SF  denotes the severity factor
a large early release of radiation because Wolf Creek has a large, dry containment and
the accident sequences contributing to a change in the core damage frequency did not
involve either a steam generator tube rupture or an intersystem loss of coolant accident.
n
Since this bounding change in core damage frequency was less than 1E-6/year and the
Suppressio
finding did not involve a significant increase in the risk of a large early release frequency,
Non
the inspectors determined this performance deficiency had very low risk significance
P
(Green). This finding was not assigned a cross-cutting aspect because it existed more
than two years and does not represent current performance.
As a compensatory measure, the licensee implemented an hourly fire watch in the
affected fire areas, with the exception of the reactor building, which is not readily
accessible during power operations. For the reactor building, the licensee is monitoring
the containment temperature as a compensatory measure.
Enforcement. License Condition 2.C.(5) states, in part, that the licensee shall maintain
in effect all provisions of the approved fire protection program as described in the
Standardized Nuclear Unit Power Plant System (SNUPPS) Final Safety Analysis Report
for the facility through Revision 17, the Wolf Creek Site Addendum through Revision 15,
and as approved in the Safety Evaluation Report through Supplement 5. The Wolf
Creek Updated Safety Analysis Report combined the SNUPPS Final Safety Analysis
Report, Revision 17, and the Wolf Creek Site Addendum, Revision 15, into one
document.
Appendix 9.5B of the Updated Safety Analysis Report provides an area-by-area analysis
of the power block that incorporated Drawing E-1F9905, Fire Hazards Analysis,
Revision 2, by reference. Drawing E-1F9905 states that the overall intent is to
demonstrate that a single plant fire will not negatively affect the post-fire safe shutdown
capability and that if a circuit damaged by a fire is protected by an individual overcurrent
protection device, that device is assumed to function to clear the fault.
Contrary to the above, prior to December 22, 2009, the licensee failed to implement and
maintain in effect all provisions of the approved fire protection program. Specifically, the
licensee prescribed mitigating actions in response to certain fire scenarios that would
result in a loss of circuit breaker coordination (i.e., disable an overcurrent protection
device from functioning to clear a fault) and could initiate secondary fires in plant
locations outside of the initial fire area that negatively affect the post-fire safe shutdown
capability. However, the plants post-fire safe shutdown capability only evaluated
damage resulting from a single fire.
                                      - 75 -                                    Enclosure 2


  The licensee entered this issue into their corrective action program as Performance
denotes the non-suppression probability
  Improvement Request 2008-005210. Because this violation was of very low safety
  significance and it was entered into the corrective action program, this violation is being
  treated as a non-cited violation, consistent with the NRC Enforcement Policy:
  NCV 05000482/2009005-16, Operator Actions Disable Circuit Breaker Coordination and
  Could Initiate Secondary Fires.
.4 (Closed) Unresolved Item 05000482/2008010-01: Post-fire Safe Shutdown Inspection
  Did Not Identify Diagnostic Information
  During a triennial fire protection inspection in 2008, the inspectors identified an
  unresolved item concerning the availability of diagnostic instrumentation needed to
  respond to a loss of reactor coolant pump seal cooling during certain fire scenarios. The
  plant design uses reactor coolant pump seal injection and thermal barrier cooling to cool
  the reactor coolant pump seals. One method of seal cooling must be maintained during
  reactor coolant pump operation to prevent seal failure, which, in some cases, could lead
  to increased seal leakage beyond the capacity of the charging pump.
  The licensee identified that fire damage in four fire areas could isolate both methods of
  seal cooling. The inspectors identified that the licensee relied upon a decrease in
  pressurizer level to diagnose a loss of seal cooling. The inspectors determined the fire
  response procedure was inadequate since pressurizer level would not decrease until
  after seal failure occurred. Since the procedure required operators to recognize the loss
  of cooling and take response actions and the procedure did not identify adequate
  instrumentation to be used, the inspectors could not verify that it would remain free of
  fire damage for fires in these four fire areas.
  In response to the unresolved item, the licensee determined the instrumentation that
  would be available to diagnose a loss of seal cooling for fires in these four areas. The
  licensee determined that the thermal barrier flow switches and alarms would remain
  available for all four areas. The licensee also determined that seal injection flow and
  temperature would remain available for most, if not all, of the trains for each fire area.
  The inspectors reviewed the abnormal operating procedures used in the event of reactor
  coolant pump problems. Based on this review and the licensees analysis of available
  instrumentation, the inspectors concluded that it was reasonable to believe that
  operators had sufficient instrumentation and guidance to promptly recognize, diagnose,
  and respond to a loss of reactor coolant pump seal cooling.
  The failure to establish written procedures adequately implementing the approved fire
  protection program was a performance deficiency and a violation of Technical
  Specification 5.4.1.d. The inspectors determined this performance deficiency was of
  minor safety significance since it was not similar to any example in Manual
  Chapter 0612, Appendix E, nor did it meet any of the minor questions in Manual
  Chapter 0612, Appendix B. This performance deficiency constitutes a violation of minor
  significance that is not subject to enforcement action in accordance with the NRCs
  Enforcement Policy.
                                        - 76 -                                    Enclosure 2


    The licensee implemented an hourly fire watch as an immediate compensatory measure
    and entered this issue into their corrective action program as Condition
    Report 2008-005171.
- 75 -
.5  (Closed) Licensee Event Report 05000482/2008006-00: Entry Into Mode 4 Without An
    Operable Containment Spray System
    On July 3, 2008, Wolf Creek submitted LER 2008006 which described missed VT-2 weld
    inspections when modifying train B containment spray recirculation line in refueling
    outage 16. Wolf Creek stated that changes to shim the recirculation line inadvertently
Enclosure 2
    resulted in missing the VT-2 post-maintenance test. This resulted in ascending to Mode
    4 without an operable containment spray system. Wolf Creek identified this issue on
    May 8, 2008, at 1:45am and entered Technical Specification 3.6.6 while in Mode 4. The
Short
    VT-2 inspections were performed satisfactorily and Technical Specification 3.6.6 was
Hot
    exited at 3:13am on May 8, 2008. Enforcement aspects are discussed in Section 4OA7.
P
    This LER is closed.
denotes the probability of a hot short
.6  (Closed) Licensee Event Report 05000482/2008-08-00, -01, -02: Potential for Residual
The sum of the conditional core damage probabilities for each of the fire scenarios
    Heat Removal Trains to be Inoperable during Mode Change.
bounded the total change in core damage frequency associated with this performance
    All three revisions of this licensee event report were discussed and enforcement action
deficiency.  Since the change in core damage frequency exceeded1E-7, the inspectors
    was taken in NRC Inspection Report 05000482/2009006. This licensee event report is
screened the finding for its potential risk contribution to a large early release frequency.  
    closed.
In accordance with the guidance in NRC Inspection Manual Chapter 0609, Appendix H,  
.(Closed) Unresolved Item 2008005-02: Residual Heat Removal Suction Piping
the inspectors determined this finding did not involve a significant increase in the risk of
    Saturation Temperature and Pressure.
a large early release of radiation because Wolf Creek has a large, dry containment and
    This unresolved item was inspected and enforcement action was taken in NRC
the accident sequences contributing to a change in the core damage frequency did not
    Inspection Report 05000482/2009006. This unresolved item is closed.
involve either a steam generator tube rupture or an intersystem loss of coolant accident.  
.8  (Closed) Licensee Event Report 05000482/2008-004-01: Loss of Power Event When
Since this bounding change in core damage frequency was less than 1E-6/year and the
    the Reactor was Defueled.
finding did not involve a significant increase in the risk of a large early release frequency,  
    Licensee Event Report 05000482/2008-004-00 was closed in NRC Inspection
the inspectors determined this performance deficiency had very low risk significance
    Report 05000482/2008004 as a Green finding. In NRC Inspection
(Green).  This finding was not assigned a cross-cutting aspect because it existed more
    Report 05000482/2009004, the inspectors identified a violation of 10 CFR 50.73
than two years and does not represent current performance.  
    associated with this event report. Wolf Creek subsequently submitted revised Licensee
As a compensatory measure, the licensee implemented an hourly fire watch in the
    Event Report 2008-004-01 in response to the Severity Level IV violation. The submittal
affected fire areas, with the exception of the reactor building, which is not readily
    of Licensee Event Report 05000482/2008-004-01 restores compliance with
accessible during power operations. For the reactor building, the licensee is monitoring
    10 CFR 50.73. This licensee event report is closed.
the containment temperature as a compensatory measure.  
4OA6 Meetings
Enforcement.  License Condition 2.C.(5) states, in part, that the licensee shall maintain
    Exit Meeting Summary
in effect all provisions of the approved fire protection program as described in the
    On October 22, 2009, the radiation protection inspectors presented the inspection results
Standardized Nuclear Unit Power Plant System (SNUPPS) Final Safety Analysis Report  
    to Mr. M. W. Sunseri and other members of the licensee staff. The licensee
for the facility through Revision 17, the Wolf Creek Site Addendum through Revision 15,
                                          - 77 -                                Enclosure 2
and as approved in the Safety Evaluation Report through Supplement 5.  The Wolf
Creek Updated Safety Analysis Report combined the SNUPPS Final Safety Analysis
Report, Revision 17, and the Wolf Creek Site Addendum, Revision 15, into one
document.  
Appendix 9.5B of the Updated Safety Analysis Report provides an area-by-area analysis
of the power block that incorporated Drawing E-1F9905, Fire Hazards Analysis,
Revision 2, by reference. Drawing E-1F9905 states that the overall intent is to
demonstrate that a single plant fire will not negatively affect the post-fire safe shutdown
capability and that if a circuit damaged by a fire is protected by an individual overcurrent
protection device, that device is assumed to function to clear the fault.
Contrary to the above, prior to December 22, 2009, the licensee failed to implement and
maintain in effect all provisions of the approved fire protection program.  Specifically, the  
licensee prescribed mitigating actions in response to certain fire scenarios that would
result in a loss of circuit breaker coordination (i.e., disable an overcurrent protection
device from functioning to clear a fault) and could initiate secondary fires in plant
locations outside of the initial fire area that negatively affect the post-fire safe shutdown
capability. However, the plants post-fire safe shutdown capability only evaluated
damage resulting from a single fire.


        acknowledged the issues presented. The inspector asked the licensee whether any
        materials examined during the inspection should be considered proprietary. No
        proprietary information was identified.
- 76 -
        On October 30, 2009, the in-service inspection inspectors debriefed the inspection
        results to Mr. M. W. Sunseri, and other members of the licensee staff. The licensee
        acknowledged the issues presented. The inspectors acknowledged review of proprietary
        material during the inspection which had been or will be returned to the licensee.
        On December 17 and 22, the fire protection inspectors conducted telephonic exit
Enclosure 2
        meetings and presented the results of the staffs closure of fire protection unresolved
The licensee entered this issue into their corrective action program as Performance
        items. The inspectors presented the results to L. Ratzlaff, Manager Support
Improvement Request 2008-005210. Because this violation was of very low safety
        Engineering, on December 17 and M.W. Sunseri, on December 22. The licensee
significance and it was entered into the corrective action program, this violation is being
        acknowledged the issues presented. The inspectors asked the licensee whether any of
treated as a non-cited violation, consistent with the NRC Enforcement Policy:
        the material examined during the inspection should be considered proprietary. No
NCV 05000482/2009005-16, Operator Actions Disable Circuit Breaker Coordination and  
        proprietary information was identified.
Could Initiate Secondary Fires.  
        On January 14, 2010, the resident inspectors presented the inspection results of the
        resident inspections to Mr. M.W. Sunseri, and other members of the licensee's
.4
        management staff. The licensee acknowledged the findings presented. The inspectors
(Closed) Unresolved Item 05000482/2008010-01:  Post-fire Safe Shutdown Inspection 
        noted that while proprietary information was reviewed, none would be included in this
Did Not Identify Diagnostic Information
        report.
During a triennial fire protection inspection in 2008, the inspectors identified an
4OA7 Licensee-Identified Violations
unresolved item concerning the availability of diagnostic instrumentation needed to
The following violations of very low safety significance (Green) were identified by the licensee
respond to a loss of reactor coolant pump seal cooling during certain fire scenarios. The  
and are violations of NRC requirements which meet the criteria of Section VI of the NRC
plant design uses reactor coolant pump seal injection and thermal barrier cooling to cool
Enforcement Policy, NUREG-1600, for being dispositioned as noncited violations.
the reactor coolant pump seals.  One method of seal cooling must be maintained during
.1      On October 22, 2009, at 12:06 p.m., the Wolf Creek control room received trouble
reactor coolant pump operation to prevent seal failure, which, in some cases, could lead
        annunciators for emergency diesel generator A. Emergency diesel generator B was out
to increased seal leakage beyond the capacity of the charging pump.  
        of service for planned maintenance. 10 CFR 50.47(b)(4) requires that a standard
The licensee identified that fire damage in four fire areas could isolate both methods of
        emergency classification action level scheme be used by the licensee. Wolf Creek
seal cooling. The inspectors identified that the licensee relied upon a decrease in
        EAL 6, Loss of Electrical Power/Assessment Capability, requires, in part, that when
pressurizer level to diagnose a loss of seal cooling.  The inspectors determined the fire
        both emergency diesel generators are out of service for greater than 15 minutes, a
response procedure was inadequate since pressurizer level would not decrease until
        Notice of Unusual Event be declared. Contrary to the above, on October 22, 2009, Wolf
after seal failure occurred. Since the procedure required operators to recognize the loss
        Creek did not declare a Notice of Unusual Event until 5 hours after both emergency
of cooling and take response actions and the procedure did not identify adequate
        diesel generators were out of service. This issue is of very low safety significance
instrumentation to be used, the inspectors could not verify that it would remain free of  
        (Green) because it is associated with failure to report a Notification of Unusual Event.
fire damage for fires in these four fire areas.  
        Wolf Creek initiated Condition Report 21058 regarding the late declaration.
In response to the unresolved item, the licensee determined the instrumentation that
.2      On July 3, 2008, Wolf Creek submitted Licensee Event Report LER 2008006 which
would be available to diagnose a loss of seal cooling for fires in these four areas. The  
        described missed VT-2 weld inspections when modifying train B containment spray
licensee determined that the thermal barrier flow switches and alarms would remain
        recirculation line in Refueling Outage 16, requiring the train to be declared inoperable.
available for all four areas. The licensee also determined that seal injection flow and  
        This issue has been entered in to the corrective action program as Condition
temperature would remain available for most, if not all, of the trains for each fire area.  
        Report 2008-2197. Technical Specification 3.0.4, states, in part, that when a limiting
The inspectors reviewed the abnormal operating procedures used in the event of reactor
        condition of operation is not met, that mode changes shall only be made: when actions
coolant pump problems. Based on this review and the licensees analysis of available
        to be entered permit continued operation for an unlimited period of time, after a risk
instrumentation, the inspectors concluded that it was reasonable to believe that
                                            - 78 -                                    Enclosure 2
operators had sufficient instrumentation and guidance to promptly recognize, diagnose,  
and respond to a loss of reactor coolant pump seal cooling.  
The failure to establish written procedures adequately implementing the approved fire
protection program was a performance deficiency and a violation of Technical
Specification 5.4.1.d.  The inspectors determined this performance deficiency was of  
minor safety significance since it was not similar to any example in Manual
Chapter 0612, Appendix E, nor did it meet any of the minor questions in Manual
Chapter 0612, Appendix B. This performance deficiency constitutes a violation of minor
significance that is not subject to enforcement action in accordance with the NRCs
Enforcement Policy.


assessment, or when an allowance is stated in the specification. Technical Specification
Limiting Condition of Operation 3.6.6 requires, in part, two operable trains of
containment spray in Modes 1 through 4. Contrary to the above, on May 8, 2008, Wolf
- 77 -
Creek entered Mode 4 with only one operable containment spray system. This issue is
of very low safety significance (Green) because there was no loss of function of the
Enclosure 2
The licensee implemented an hourly fire watch as an immediate compensatory measure
and entered this issue into their corrective action program as Condition
Report 2008-005171.
.5
(Closed) Licensee Event Report 05000482/2008006-00:  Entry Into Mode 4 Without An
Operable Containment Spray System
On July 3, 2008, Wolf Creek submitted LER 2008006 which described missed VT-2 weld
inspections when modifying train B containment spray recirculation line in refueling
outage 16.  Wolf Creek stated that changes to shim the recirculation line inadvertently
resulted in missing the VT-2 post-maintenance test.  This resulted in ascending to Mode
4 without an operable containment spray system.  Wolf Creek identified this issue on
May 8, 2008, at 1:45am and entered Technical Specification 3.6.6 while in Mode 4.  The
VT-2 inspections were performed satisfactorily and Technical Specification 3.6.6 was
exited at 3:13am on May 8, 2008.  Enforcement aspects are discussed in Section 4OA7. 
This LER is closed.
.6
(Closed) Licensee Event Report 05000482/2008-08-00, -01, -02:  Potential for Residual
Heat Removal Trains to be Inoperable during Mode Change.
All three revisions of this licensee event report were discussed and enforcement action
was taken in NRC Inspection Report 05000482/2009006.  This licensee event report is
closed.
.7
(Closed) Unresolved Item 2008005-02:  Residual Heat Removal Suction Piping
Saturation Temperature and Pressure.
This unresolved item was inspected and enforcement action was taken in NRC
Inspection Report 05000482/2009006.  This unresolved item is closed.
.8
(Closed) Licensee Event Report 05000482/2008-004-01:  Loss of Power Event When
the Reactor was Defueled.
Licensee Event Report 05000482/2008-004-00 was closed in NRC Inspection
Report 05000482/2008004 as a Green finding.  In NRC Inspection
Report 05000482/2009004, the inspectors identified a violation of 10 CFR 50.73
associated with this event report.  Wolf Creek subsequently submitted revised Licensee
Event Report 2008-004-01 in response to the Severity Level IV violation.  The submittal
of Licensee Event Report 05000482/2008-004-01 restores compliance with
10 CFR 50.73.  This licensee event report is closed. 
4OA6 Meetings 
Exit Meeting Summary
On October 22, 2009, the radiation protection inspectors presented the inspection results
to Mr. M. W. Sunseri and other members of the licensee staff.  The licensee
 
- 78 -
Enclosure 2
acknowledged the issues presented.  The inspector asked the licensee whether any
materials examined during the inspection should be considered proprietary.  No
proprietary information was identified.
On October 30, 2009, the in-service inspection inspectors debriefed the inspection
results to Mr. M. W. Sunseri, and other members of the licensee staff.  The licensee
acknowledged the issues presented.  The inspectors acknowledged review of proprietary
material during the inspection which had been or will be returned to the licensee. 
On December 17 and 22, the fire protection inspectors conducted telephonic exit
meetings and presented the results of the staffs closure of fire protection unresolved
items.  The inspectors presented the results to L. Ratzlaff, Manager Support
Engineering, on December 17 and M.W. Sunseri, on December 22.  The licensee
acknowledged the issues presented.  The inspectors asked the licensee whether any of
the material examined during the inspection should be considered proprietary.  No
proprietary information was identified.
On January 14, 2010, the resident inspectors presented the inspection results of the
resident inspections to Mr. M.W. Sunseri, and other members of the licensee's
management staff.  The licensee acknowledged the findings presented.  The inspectors
noted that while proprietary information was reviewed, none would be included in this
report.
4OA7 Licensee-Identified Violations 
The following violations of very low safety significance (Green) were identified by the licensee
and are violations of NRC requirements which meet the criteria of Section VI of the NRC
Enforcement Policy, NUREG-1600, for being dispositioned as noncited violations.
.1
On October 22, 2009, at 12:06 p.m., the Wolf Creek control room received trouble
annunciators for emergency diesel generator A.  Emergency diesel generator B was out
of service for planned maintenance.  10 CFR 50.47(b)(4) requires that a standard
emergency classification action level scheme be used by the licensee.  Wolf Creek
EAL 6, Loss of Electrical Power/Assessment Capability, requires, in part, that when
both emergency diesel generators are out of service for greater than 15 minutes, a
Notice of Unusual Event be declared.  Contrary to the above, on October 22, 2009, Wolf
Creek did not declare a Notice of Unusual Event until 5 hours after both emergency
diesel generators were out of service.  This issue is of very low safety significance
(Green) because it is associated with failure to report a Notification of Unusual Event. 
Wolf Creek initiated Condition Report 21058 regarding the late declaration. 
.2
On July 3, 2008, Wolf Creek submitted Licensee Event Report LER 2008006 which
described missed VT-2 weld inspections when modifying train B containment spray
recirculation line in Refueling Outage 16, requiring the train to be declared inoperable. 
This issue has been entered in to the corrective action program as Condition
Report 2008-2197.  Technical Specification 3.0.4, states, in part, that when a limiting
condition of operation is not met, that mode changes shall only be made: when actions
to be entered permit continued operation for an unlimited period of time, after a risk
 
- 79 -
Enclosure 2
assessment, or when an allowance is stated in the specification. Technical Specification  
Limiting Condition of Operation 3.6.6 requires, in part, two operable trains of  
containment spray in Modes 1 through 4. Contrary to the above, on May 8, 2008, Wolf  
Creek entered Mode 4 with only one operable containment spray system. This issue is  
of very low safety significance (Green) because there was no loss of function of the  
containment spray system.
containment spray system.
                                  - 79 -                                    Enclosure 2


                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee Personnel
A-1
R. D. Benham, Integrated Plant Scheduling
T. D. Card, Engineering
B. E. Dale, Manager Maintenance
T. M. Damashek, Superintendent, Operations Support
T. F. East, Manager, Emergency Planning
Attachment 1
D. L. Fehr, Manager Information Systems
SUPPLEMENTAL INFORMATION  
R. L. Gardner, Manager, Quality
KEY POINTS OF CONTACT
S. E. Hedges, Vice President Oversight
Licensee Personnel  
D. M Hooper, Supervisor Licensing
R. D. Benham, Integrated Plant Scheduling  
J. K. Kent, Finance Management
T. D. Card, Engineering  
W. R. Ketchum, Supervisor, Plant Safety Assessment
B. E. Dale, Manager Maintenance  
S. R. Koenig, Corrective Actions
T. M. Damashek, Superintendent, Operations Support  
W. T. Muilenburg, Licensing
T. F. East, Manager, Emergency Planning  
P. J. Bedgood, Superintendent, Chemistry/Radiation Protection
D. L. Fehr, Manager Information Systems  
C. L. Palmer, Major Modifications
R. L. Gardner, Manager, Quality  
J. M. Pankaskie, Supervisor, Design Engineering
S. E. Hedges, Vice President Oversight  
E. M. Peterson, Ombudsman
D. M Hooper, Supervisor Licensing  
D. Phelps, Owners Representative
J. K. Kent, Finance Management  
B. Poteat, Piedmont
W. R. Ketchum, Supervisor, Plant Safety Assessment  
L. Ratzlaff, Manager, Support Engineering
S. R. Koenig, Corrective Actions  
E. A. Ray, Manager Chemistry/Health Physics
W. T. Muilenburg, Licensing  
K. Scherich, Director Engineering
P. J. Bedgood, Superintendent, Chemistry/Radiation Protection  
A. F. Stull, Vice President & Chief Administrative Officer
C. L. Palmer, Major Modifications  
M. W. Sunseri, President and Chief Executive Officer
J. M. Pankaskie, Supervisor, Design Engineering  
B. J. Vickery, Supply Chain
E. M. Peterson, Ombudsman  
B. Walters, Supervisor, Security
D. Phelps, Owners Representative  
M. J. Westman, Manager, Training
B. Poteat, Piedmont  
K. Frederickson, Licensing
L. Ratzlaff, Manager, Support Engineering  
J. Suter, Fire Protection
E. A. Ray, Manager Chemistry/Health Physics  
NRC Personnel
K. Scherich, Director Engineering  
D. Loveless, Senior Reactor Analyst
A. F. Stull, Vice President & Chief Administrative Officer  
                                          A-1               Attachment 1
M. W. Sunseri, President and Chief Executive Officer
B. J. Vickery, Supply Chain  
B. Walters, Supervisor, Security  
M. J. Westman, Manager, Training  
K. Frederickson, Licensing  
J. Suter, Fire Protection  
NRC Personnel  
D. Loveless, Senior Reactor Analyst  
 
A-2
Attachment 1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
05000482/2009005-02
NCV
Control of Transient Ignition Sources (Section 1R05)
05000482/2009005-03
NCV
Failure to Identify Sources of Boron Leakage
(Section 1R08)
05000482/2009005-04
NCV
Failure to Incorporate Requirements of Regulatory
Guide 1.182 into Daily Shutdown Risk Assessment
(Section 1R13.1)
05000482/2009005-05
NCV
Mode Change Under Technical Specification 3.0.4.b
Without Required Risk Management Actions
(Section 1R13.2)
05000482/2009005-06
NCV
Failure to Follow Corrective Action Procedure
(Section 1R13.3)
05000482/2009005-07
NCV
Failure to Follow Procedure Results in Draining of
Emergency Core Cooling System Pump Oil
(Section 1R13.4)
05000482/2009005-08
NCV
Inadequate Operability Evaluation of Essential Service
Water Pumps (Section 1R15.1)
05000482/2009005-09
NCV
Positive Reactivity Addition Prohibited by Technical
Specifications while in Mode 2 (Section 1R15.2)
05000482/2009005-10
NCV
Failure to Obtain Vendor Data Necessary for Plant
Modification (Section 1R18)
05000482/2009005-12
NCV
Unevaluated Scaffold Against Component Cooling Water
Piping (Section 1R20)
05000482/2009005-13
NCV
Failure to Maintain Administrative Control of Keys to
Locked High Radiation Areas (Section 2SO1)
05000482/2009005-14
NCV
Failure to Identify Inoperable P-6 Interlock and
Intermediate Range Detector (Section 4OA2)
05000482/2009005-15
NCV
Failure to Report a Condition that Could Have Prevented
Fulfillment of a Safety Function (Section 4OA3)
05000482/2009005-16
NCV
Operator Actions disable Circuit Breaker Coordination and
Could Initiate Secondary Fires (Section 4OA5.1)
 
A-3
Attachment 1  
Opened
05000482/2009005-01
VIO
Failure to Correct Discolored Boric Acid Deposits
(Section 1R05)
05000482/2009005-11
VIO
Failure to Correct Vessel Head Vent Path (Section 1R20)
Discussed
05000482/2009002-07
VIO
Failure to correct component cooling water valve closures
(EA-09-110) (Section 1R18)
05000482/2009-005-00
LER
Loss of both Diesel Generators with all fuel in the Spent
Fuel Pool (Section 4OA3)
Closed
05000482/2008010-01
URI
Post Fire Safe Shutdown Procedure Did Not Identify
Diagnostic Information (Section 4OA5.4)
05000482/2008010-04
URI
Operator Actions May Create the Potential for Secondary
Fires (Section 4OA5.3)
05000482/2008-006-00
LER
Entry Into Mode 4 Without An Operable Containment
Spray System  (4OA5.5)
05000482/2008-008-00
05000482/2008-008-01
05000482/2008-008-02
LER
Potential for Residual Heat Removal Trains to be
Inoperable during Mode Change (Section 4OA5.6)
05000482/2008005-02
URI
Residual Heat Removal Suction Piping Saturation
Temperature and Pressure (Section 4OA5.7)
05000482/2008-004-01
LER
Loss of Power Event When the Reactor was Defueled
(Section 4OA5.8)
LIST OF DOCUMENTS REVIEWED
Section 1RO1:  Adverse Weather Protection
MISCELLANEOUS
NUMBER
TITLE
REVISION
FL-01
Flooding of Auxiliary Building
01
CR 22801
Auxiliary Building Flooding Question
3.4.1
Updated Safety Analysis Report, Flood Protection
19


                LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
  05000482/2009005-02    NCV    Control of Transient Ignition Sources (Section 1R05)
A-4
  05000482/2009005-03    NCV    Failure to Identify Sources of Boron Leakage
   
                              (Section 1R08)
   
  05000482/2009005-04    NCV    Failure to Incorporate Requirements of Regulatory
                              Guide 1.182 into Daily Shutdown Risk Assessment
   
                              (Section 1R13.1)
Attachment 1  
  05000482/2009005-05    NCV    Mode Change Under Technical Specification 3.0.4.b
Section 1RO4:  Equipment Alignment
                              Without Required Risk Management Actions
                              (Section 1R13.2)
PROCEDURES
05000482/2009005-06    NCV    Failure to Follow Corrective Action Procedure
   
                              (Section 1R13.3)
NUMBER
05000482/2009005-07    NCV    Failure to Follow Procedure Results in Draining of
TITLE
                              Emergency Core Cooling System Pump Oil
REVISION
                              (Section 1R13.4)
M-12EC01
  05000482/2009005-08    NCV    Inadequate Operability Evaluation of Essential Service
Fuel Pool Cooling and Clean-up System
                              Water Pumps (Section 1R15.1)
19
  05000482/2009005-09    NCV    Positive Reactivity Addition Prohibited by Technical
SYS EC-120
                              Specifications while in Mode 2 (Section 1R15.2)
Fuel Pool Cooling and Clean-up System Startup
  05000482/2009005-10    NCV    Failure to Obtain Vendor Data Necessary for Plant
44
                              Modification (Section 1R18)
CKL EC-120
  05000482/2009005-12    NCV    Unevaluated Scaffold Against Component Cooling Water
Fuel Pool Cooling and Clean-up System Normal
                              Piping (Section 1R20)
Valve Lineup/Breaker Checklist
  05000482/2009005-13    NCV    Failure to Maintain Administrative Control of Keys to
14A
                              Locked High Radiation Areas (Section 2SO1)
CKL JE-120
  05000482/2009005-14    NCV    Failure to Identify Inoperable P-6 Interlock and
Emergency Fuel Oil System Lineup
                              Intermediate Range Detector (Section 4OA2)
19
  05000482/2009005-15    NCV    Failure to Report a Condition that Could Have Prevented
STS NB-005
                              Fulfillment of a Safety Function (Section 4OA3)
Breaker Alignment Verification
  05000482/2009005-16    NCV    Operator Actions disable Circuit Breaker Coordination and
18
                              Could Initiate Secondary Fires (Section 4OA5.1)
CKL KJ-121
                                      A-2                                    Attachment 1
Diesel Generator NE01 and NE02 Valve Checklist
28A
FPPM-015
Fuel Building Elevation 2000 
7
Section 1RO5:  Fire Protection
   
PROCEDURES
   
NUMBER
TITLE
REVISION
FPPM-009
Control Bldg El. 2000
2  
AP 10-106
Fire Preplans 
   
7
Fppm-015
Fuel Building Elevation 2000
7
Section 1RO6:  Flood Protection Measures
MISCELLANEOUS
   
NUMBER
TITLE
ALR 00-095C
AFP Sump Room Level Hi
   
FL-14
Feed Pump Room Maximum Flood Level
   
LE-M-002
Auxiliary Building Room 1206, 1207 Maximum Flood
Level
   
WORK ORDER
   
WO 08-304475-000


Opened
  05000482/2009005-01  VIO      Failure to Correct Discolored Boric Acid Deposits
   
                                (Section 1R05)
A-5
  05000482/2009005-11  VIO      Failure to Correct Vessel Head Vent Path (Section 1R20)
Discussed
   
  05000482/2009002-07  VIO      Failure to correct component cooling water valve closures
                                (EA-09-110) (Section 1R18)
   
  05000482/2009-005-00 LER      Loss of both Diesel Generators with all fuel in the Spent
Attachment 1
                                Fuel Pool (Section 4OA3)
Section 1RO7:  Heat Sink Performance
Closed
  05000482/2008010-01  URI      Post Fire Safe Shutdown Procedure Did Not Identify
PROCEDURES
                                Diagnostic Information (Section 4OA5.4)
   
  05000482/2008010-04  URI      Operator Actions May Create the Potential for Secondary
NUMBER
                                Fires (Section 4OA5.3)
TITLE
  05000482/2008-006-00 LER      Entry Into Mode 4 Without An Operable Containment
REVISION
                                Spray System (4OA5.5)
STN PE-038
  05000482/2008-008-00  LER      Potential for Residual Heat Removal Trains to be
Containment Cooler Performance Test
05000482/2008-008-01          Inoperable during Mode Change (Section 4OA5.6)
10
05000482/2008-008-02
EPRI NP-7552
05000482/2008005-02  URI      Residual Heat Removal Suction Piping Saturation
Heat Exchanger Performance Monitoring Guidelines
                                Temperature and Pressure (Section 4OA5.7)
1991
  05000482/2008-004-01  LER      Loss of Power Event When the Reactor was Defueled
   
                                (Section 4OA5.8)
Section 1RO8:  Inservice Inspection Activities
                        LIST OF DOCUMENTS REVIEWED
Section 1RO1: Adverse Weather Protection
CONDITION REPORTS 
MISCELLANEOUS
   
      NUMBER                                  TITLE                            REVISION
00003599
FL-01                Flooding of Auxiliary Building                                01
00011297
CR 22801              Auxiliary Building Flooding Question
00011954
  3.4.1                Updated Safety Analysis Report, Flood Protection            19
00018217
                                      A-3                                    Attachment 1
00018785
00019248
00020993
00021274
2008-004840
   
CONDITION REPORT GENERATED FOR THIS INSPECTION
   
00020993, Fire Watches
   
DRAWINGS
   
NUMBER
TITLE
REVISION
E 11173-171-005
Westinghouse Electric corporation General Arrangement
Plan
001
E 11373-101-005
Westinghouse Electric Corporation Closure Head
Assembly
002
E 1455E85,
Sheet 1
Westinghouse Electric Corporation Closure Head (SAP)  
General Assembly 
001
E 6467E69
Wolf Creek Simplified Head Assembly Radiation Shield
Assembly
006
M 164-00043
Mirror Insulation
W008
M-189-50EJ-02-04
Residual Heat Removal B Train RHR Pump Suction  
00
   
PROCEDURES
NUMBER
TITLE
REVISION  
AI 16F-001
Evaluation of Boric Acid Leakage
5
AI 16F-002
Boric Acid Leakage Management
5
AP 16F-001
Boric Acid Corrosion Control Program
5


Section 1RO4: Equipment Alignment
PROCEDURES
      NUMBER                                   TITLE                       REVISION
A-6
  M-12EC01              Fuel Pool Cooling and Clean-up System                    19
SYS EC-120            Fuel Pool Cooling and Clean-up System Startup            44
CKL EC-120            Fuel Pool Cooling and Clean-up System Normal            14A
                        Valve Lineup/Breaker Checklist
CKL JE-120            Emergency Fuel Oil System Lineup                        19
Attachment 1
STS NB-005            Breaker Alignment Verification                           18
NUMBER  
CKL KJ-121            Diesel Generator NE01 and NE02 Valve Checklist          28A
TITLE  
FPPM-015              Fuel Building Elevation 2000                            7
REVISION  
Section 1RO5: Fire Protection
29A-003
PROCEDURES
Steam Generator Management
      NUMBER                                  TITLE                      REVISION
   
FPPM-009              Control Bldg El. 2000                                    2
AP-10-100
AP 10-106              Fire Preplans                                            7
Fire Protection Program
Fppm-015              Fuel Building Elevation 2000                            7
14
Section 1RO6: Flood Protection Measures
AP-10-101
MISCELLANEOUS
Control of Transient Ignition Sources
      NUMBER                                  TITLE
12
ALR 00-095C            AFP Sump Room Level Hi
AP-10-102
FL-14                  Feed Pump Room Maximum Flood Level
Control of Combustible Materials
LE-M-002                Auxiliary Building Room 1206, 1207 Maximum Flood
13
                        Level
AP-21I-001
WORK ORDER
Temporary Modification
WO 08-304475-000
8
                                        A-4                              Attachment 1
APF 28D-001
Self-Assessment Process
11
PDI-ISI-254-SE-
NB
Remote Inservice Examination of Reactor Vessel
Nozzle to Safe End, Nozzle to Pipe, and Safe end to
Pipe Welds Using the Nozzle Scanner
1
PDI-UT-1
PDI Generic Inspection Procedure for the Ultrasonic
Examination of Ferritic Pipe Welds
D
PDI-UT-2
PDI Generic Inspection Procedure for the Ultrasonic
Examination of Austenitic Pipe Welds
C
PDI-UT-6
PDI Generic Inspection Procedure for the Ultrasonic
Examination of Reactor Pressure Vessel Welds
F
QCP-20-501
PT
8
QCP-20-502
MT
8
QCP-20-503
UT Thickness-Wall Thin
3
QCP-20-504
UT For Flaw Detection
5
QCP-20-508
RT Welds and Components
4
QCP-20-510
Ultrasonic Instrument Linearity Verification  
3
QCP-20-511
RT of AWS Groove Welds
1B
QCP-20-514
ET Testing
5B
QCP-20-516
PT/NON-STD Temp
05
QCP-20-517
RT Wall Thinning
2A
QCP-20-521
UT Profile and Plotting
1B
QCP-20-522
Ultrasonic Examination of Ferritic Piping Welds
1B
QCP-20-523
Ultrasonic Examination of Austenitic Piping Welds
1B
QCP-20-527
UT- Soldering
1
QCP-20-540
VT-1 Exam
0B
QCP-20-541
VT-3 Exam
2
QCP-20-543
Fluorescent Dye PT Exam
1  


Section 1RO7: Heat Sink Performance
PROCEDURES
        NUMBER                                   TITLE                       REVISION
A-7
STN PE-038              Containment Cooler Performance Test                      10
EPRI NP-7552            Heat Exchanger Performance Monitoring Guidelines      1991
Section 1RO8: Inservice Inspection Activities
CONDITION REPORTS
00003599          00011297            00011954          00018217        00018785
Attachment 1
00019248          00020993            00021274          2008-004840
NUMBER  
CONDITION REPORT GENERATED FOR THIS INSPECTION
TITLE  
00020993, Fire Watches
REVISION  
DRAWINGS
SG-CDME-08-15
    NUMBER                                  TITLE                          REVISION
Wolf Creek RF16 Condition Monitoring Assessment and
E 11173-171-005    Westinghouse Electric corporation General Arrangement        001
Operational Assessment, April 2008
                  Plan
1
E 11373-101-005    Westinghouse Electric Corporation Closure Head                002
SG-SGMP-09-9
                  Assembly
Steam Generator Degradation Assessment for Wolf
E 1455E85,        Westinghouse Electric Corporation Closure Head (SAP)          001
Creek, RF17 Refueling Outage, October 2009
Sheet 1            General Assembly
0
E 6467E69          Wolf Creek Simplified Head Assembly Radiation Shield          006
STN PE-040D
                  Assembly
RCS Pressure Boundary Integrity Walkdown
M 164-00043        Mirror Insulation                                            W008
3
M-189-50EJ-02-04  Residual Heat Removal B Train RHR Pump Suction                00
STN PE-040G
PROCEDURES
Transient Event Walkdown
    NUMBER                                   TITLE                           REVISION
0
  AI 16F-001        Evaluation of Boric Acid Leakage                              5
STS PE-040E
  AI 16F-002        Boric Acid Leakage Management                                 5
RPV Head Visual Inspection  
  AP 16F-001        Boric Acid Corrosion Control Program                           5
2
                                        A-5                                Attachment 1
UT-95
Ultrasonic Examination of Austenitic Piping Welds
3
WCRE-18
Boric Acid Corrosion Control Program Plan
1
WORK ORDERS
08-304695-000
09-313385-000
09-320908-000
09-320918-000
08-310117-000
09-318982-001
09-320910-000
09-320918-001  
08-310119-000
09-319416-002  
09-320910-001
09-320919-000
08-310136-000
09-320490-000
09-320911-000
09-321389-000
08-311159-000
09-320505-000
09-320912-000
08-311161-000
09-320891-000
09-320913-000
WORK REQUESTS
09-076556
09-076676
09-076711
09-076707
09-076561
09-076307
09-076705
09-076712
09-076710
09-076706
MISCELLANEOUS
NUMBER  
TITLE  
REVISION / DATE
   
Steam Generator data Analysis Desktop
Instruction
4
   
SGAMP Self Assessment, Steam Generator Asset
Management Program
October 17, 2008
   
Boric Acid Corrosion Control Program 2009 3rd
Quarter Inspection/Monitoring Report
October 13, 2009


  NUMBER                                 TITLE                       REVISION
29A-003        Steam Generator Management
AP-10-100      Fire Protection Program                                  14
A-8
AP-10-101      Control of Transient Ignition Sources                    12
AP-10-102      Control of Combustible Materials                        13
AP-21I-001      Temporary Modification                                    8
APF 28D-001    Self-Assessment Process                                  11
PDI-ISI-254-SE- Remote Inservice Examination of Reactor Vessel            1
Attachment 1
NB              Nozzle to Safe End, Nozzle to Pipe, and Safe end to
NUMBER  
                Pipe Welds Using the Nozzle Scanner
TITLE  
PDI-UT-1        PDI Generic Inspection Procedure for the Ultrasonic      D
REVISION / DATE
                Examination of Ferritic Pipe Welds
PDI-UT-2        PDI Generic Inspection Procedure for the Ultrasonic      C
Boric Acid Leakage Screening/Evaluation for
                Examination of Austenitic Pipe Welds
Component EMHV8888
PDI-UT-6        PDI Generic Inspection Procedure for the Ultrasonic      F
October 8, 2008
                Examination of Reactor Pressure Vessel Welds
QCP-20-501      PT                                                        8
Boric Acid Leakage Screening/Evaluation for
QCP-20-502      MT                                                        8
Component BGHCV0182
QCP-20-503      UT Thickness-Wall Thin                                    3
January 5, 2009
QCP-20-504      UT For Flaw Detection                                    5
QCP-20-508      RT Welds and Components                                  4
Boric Acid Leakage Screening/Evaluation for
QCP-20-510      Ultrasonic Instrument Linearity Verification              3
Component EP8956C
QCP-20-511      RT of AWS Groove Welds                                  1B
October 19, 2009
QCP-20-514      ET Testing                                              5B
QCP-20-516      PT/NON-STD Temp                                          05
Boric Acid Leakage Screening/Evaluation for
QCP-20-517      RT Wall Thinning                                        2A
Component EMHV8924
QCP-20-521      UT Profile and Plotting                                  1B
October 20, 2009
QCP-20-522      Ultrasonic Examination of Ferritic Piping Welds          1B
QCP-20-523      Ultrasonic Examination of Austenitic Piping Welds        1B
Boric Acid Leakage Screening/Evaluation for
QCP-20-527      UT- Soldering                                            1
Component BBPV8702A
QCP-20-540      VT-1 Exam                                                0B
October 14, 2009
QCP-20-541      VT-3 Exam                                                2
QCP-20-543      Fluorescent Dye PT Exam                                  1
Boric Acid Leakage Screening/Evaluation for
                                      A-6                          Attachment 1
Component BGHCV0128
July 9, 2009
Boric Acid Leakage Screening/Evaluation for
Component EMV0175
April 8, 2009
Boric Acid Leakage Screening/Evaluation for
Component BBC5413
April 7, 2009
Boric Acid Leakage Screening/Evaluation for
Component HETCV0250
January 13, 2009
Boric Acid Leakage Screening/Evaluation for
Component ECV0048
January 13, 2009
Boric Acid Leakage Screening/Evaluation for  
Component ECV0157
January 12, 2009
Boric Acid Leakage Screening/Evaluation for  
Component BBHV8351B
January 12, 2009
Boric Acid Leakage Screening/Evaluation for  
Component EJ8730A
January 12, 2009
Boric Acid Leakage Screening/Evaluation for
Component EJV0128
January 12, 2009
Boric Acid Leakage Screening/Evaluation for
Component EJFE0619
January 12, 2009
Boric Acid Leakage Screening/Evaluation for
Component BG8405A
January 9, 2009
Boric Acid Leakage Screening/Evaluation for
Component ENV0115
January 9, 2009
Boric Acid Leakage Screening/Evaluation for
Component BGV0526
January 8, 2009


    NUMBER                             TITLE                             REVISION
              Wolf Creek RF16 Condition Monitoring Assessment and            1
  SG-CDME-08-15
A-9
              Operational Assessment, April 2008
              Steam Generator Degradation Assessment for Wolf                0
  SG-SGMP-09-9
              Creek, RF17 Refueling Outage, October 2009
  STN PE-040D  RCS Pressure Boundary Integrity Walkdown                      3
Attachment 1
  STN PE-040G  Transient Event Walkdown                                      0
NUMBER  
  STS PE-040E  RPV Head Visual Inspection                                    2
TITLE  
UT-95        Ultrasonic Examination of Austenitic Piping Welds              3
REVISION / DATE
WCRE-18      Boric Acid Corrosion Control Program Plan                      1
WORK ORDERS
Boric Acid Leakage Screening/Evaluation for
  08-304695-000      09-313385-000        09-320908-000          09-320918-000
Component BBV0357
  08-310117-000      09-318982-001        09-320910-000          09-320918-001
January 5, 2009
  08-310119-000      09-319416-002        09-320910-001           09-320919-000
   
08-310136-000      09-320490-000        09-320911-000          09-321389-000
Boric Acid Leakage Screening/Evaluation for
08-311159-000      09-320505-000        09-320912-000
Component BGFCV0110A
  08-311161-000      09-320891-000        09-320913-000
January 59, 2009
WORK REQUESTS
09-076556        09-076676              09-076711              09-076707
Boric Acid Leakage Screening/Evaluation for  
09-076561        09-076307              09-076705              09-076712
Component BBV0007
09-076710        09-076706
October 15, 2009
MISCELLANEOUS
   
      NUMBER                            TITLE                        REVISION / DATE
Ultrasonic Instrument Calibration Data Record and
                  Steam Generator data Analysis Desktop                      4
Certification for Panametrics, Epoch 4,
                  Instruction
SN 081574401
                  SGAMP Self Assessment, Steam Generator Asset        October 17, 2008
September 2, 2009  
                  Management Program
   
                  Boric Acid Corrosion Control Program 2009 3rd      October 13, 2009
Transducer Certification for Krautkramer, 113-222-
                  Quarter Inspection/Monitoring Report
591, SN 00V0JM
                                    A-7                                Attachment 1
April 26, 2002
   
Transducer Certification for Krautkramer, 113-222-
591, SN 00V49N
May 16, 2002
   
Thermometer Certification for PTC, 312F,
SNs 265095, 265109, 265113
January 6, 2009
   
Krautkramer Transducer Certification, 113-224-
5591, SN SC0123
January 11, 2008
   
Krautkramer Transducer Certificate of Conformity,
113-234-591, SN SD0172
December 3, 2007
   
Ultrasonic Instrument Calibration Data Record and
Certification for Krautkramer, USN 60 SW, SN
01R5NW
August 24, 2009
APF 28D-001-02
Self Assessment Report SEL 04-038 , Steam
Generator Program
4
APF-10-102-01
Transient Combustible Materials Permit
3
AWJ003
Ultrasonic Calibration/Examination Sheet for RPV
Meridonal Weld, ISI Number CH-101-104-C
October 22, 2009
AWJ004
Ultrasonic Calibration/Examination Sheet for RPV
Meridonal Weld, ISI Number CH-101-104-B  
October 22, 2009
ET 05-0014
Docket 50-482:  10 CFR 50.55a Request Number
I3R-03 for the Third Ten-Year Interval Inservice
Inspection (ISI) Program - Request for Relief to
Allow Use of Alternate Requirements for Snubber
Inspection and Testing
September 28, 2005
ET 06-0010
Docket 50-482:  Inservice Inspection Program Plan
for the Third Ten-Year Interval and 10 CFR 50.55a
Requests I3R-01, I3R-02, and I3R-04
March 2, 2006


NUMBER                     TITLE                 REVISION / DATE
      Boric Acid Leakage Screening/Evaluation for October 8, 2008
      Component EMHV8888
A-10
      Boric Acid Leakage Screening/Evaluation for January 5, 2009
      Component BGHCV0182
      Boric Acid Leakage Screening/Evaluation for October 19, 2009
      Component EP8956C
      Boric Acid Leakage Screening/Evaluation for October 20, 2009
Attachment 1
      Component EMHV8924
NUMBER  
      Boric Acid Leakage Screening/Evaluation for October 14, 2009
TITLE  
      Component BBPV8702A
REVISION / DATE  
      Boric Acid Leakage Screening/Evaluation for   July 9, 2009
ET 06-0021
      Component BGHCV0128
Docket No. 50-482: 10 CFR 50.55a Request I3R-
      Boric Acid Leakage Screening/Evaluation for    April 8, 2009
05, Installation and Examination of Full Structural
      Component EMV0175
Weld Overlays for Repairing/Mitigating Pressurizer
      Boric Acid Leakage Screening/Evaluation for   April 7, 2009
Nozzle-to-Safe End Dissimilar Metal Welds and
      Component BBC5413
Adjacent Safe End-to-Piping Stainless Steel Welds 
      Boric Acid Leakage Screening/Evaluation for January 13, 2009
May 19. 2006
      Component HETCV0250
ET 06-0042
      Boric Acid Leakage Screening/Evaluation for January 13, 2009
Docket 50-482: Wolf Creek Nuclear Operating
      Component ECV0048
Corporations Response to the September 20,  
      Boric Acid Leakage Screening/Evaluation for January 12, 2009
2006 NRC Request for Additional Information
      Component ECV0157
Regarding 10 CFR 50.55a Request I3R-05
      Boric Acid Leakage Screening/Evaluation for January 12, 2009
September 27, 2006
      Component BBHV8351B
ET 06-0043 
      Boric Acid Leakage Screening/Evaluation for January 12, 2009
Docket 50-482:  Wolf Creek Nuclear Operating
      Component EJ8730A
Corporations Response to NRC Request for  
      Boric Acid Leakage Screening/Evaluation for January 12, 2009
Additional Information Regarding 10 CFR 50.55a
      Component EJV0128
Request I3R-01
      Boric Acid Leakage Screening/Evaluation for January 12, 2009
October 5, 2006
      Component EJFE0619
ET 06-0044
      Boric Acid Leakage Screening/Evaluation for January 9, 2009
Docket 50-482:  Wolf Creek Nuclear Operating
      Component BG8405A
Corporations Revised Commitment Regarding 10
      Boric Acid Leakage Screening/Evaluation for January 9, 2009
CFR 50.55a Request I3R-05
      Component ENV0115
October 2, 2006
      Boric Acid Leakage Screening/Evaluation for  January 8, 2009
ET 06-0058
      Component BGV0526
Docket No. 50-482:  Wolf Creek Nuclear Operating
                      A-8                          Attachment 1
Corporations Response to the Second NRC
Request for Additional Information Regarding 10
CFR 50.55a Request I3R-01
December 20, 2006
ET 08-0044
Docket No. 50-482:  10 CFR 50.55a Request I3R-
06, Alternative to Examination Requirements of
ASME Section XI for Class 1 Piping Welds
Examined from the Inside of the Reactor Vessel
September 16, 2008
ET 09-0016
Docket No. 50-482:  Revision to Technical
Specifications 5.5.9, Steam Generator (SG)
Program, and TS 5.6.10, Steam Generator Tube
Inspection Report, for a Permanent Alternate
Repair Criterion
June 2. 2009  
ET 09-0021
Docket No. 50-482:  Response to Request for  
Additional Information Related to License
Amendment Request for a Permanent Alternate
Repair Criterion to Technical Specification 5.5.9,  
Steam Generator (SG) Program
August 25, 2009  
ET 09-0023
Docket No. 50-482:  Response to Request for  
Additional Information Related to License
Amendment Request for a Permanent Alternate
Repair Criterion to Technical Specification 5.5.9,  
Steam Generator (SG) Program
September 3, 2009  


    NUMBER                           TITLE                       REVISION / DATE
              Boric Acid Leakage Screening/Evaluation for           January 5, 2009
              Component BBV0357
A-11
              Boric Acid Leakage Screening/Evaluation for          January 59, 2009
              Component BGFCV0110A
              Boric Acid Leakage Screening/Evaluation for          October 15, 2009
              Component BBV0007
              Ultrasonic Instrument Calibration Data Record and  September 2, 2009
Attachment 1
              Certification for Panametrics, Epoch 4,
NUMBER  
              SN 081574401
TITLE  
              Transducer Certification for Krautkramer, 113-222-     April 26, 2002
REVISION / DATE  
              591, SN 00V0JM
ET 09-0024
              Transducer Certification for Krautkramer, 113-222-     May 16, 2002
Docket No. 50-482:  Response to Request for
              591, SN 00V49N
Clarifications in Response to Application for  
              Thermometer Certification for PTC, 312F,              January 6, 2009
Withholding Proprietary Information from Public
              SNs 265095, 265109, 265113
Disclosure (TAC NO. ME1393)
              Krautkramer Transducer Certification, 113-224-       January 11, 2008
September 3, 2009  
              5591, SN SC0123
ET 09-0025
              Krautkramer Transducer Certificate of Conformity,  December 3, 2007
Docket No. 50-482:  Revision to Technical
              113-234-591, SN SD0172
Specification (TS) 5.5.9, Steam Generator (SG)
              Ultrasonic Instrument Calibration Data Record and    August 24, 2009
Program, and TS 5.6.10, Steam Generator Tube
              Certification for Krautkramer, USN 60 SW, SN
Inspection Report
              01R5NW
September 15, 2009  
              Self Assessment Report SEL 04-038 , Steam                    4
I-ENG-023
APF 28D-001-02
Steam Generator Data Analysis Guidelines
              Generator Program
8
APF-10-102-01  Transient Combustible Materials Permit                        3
JEW014
AWJ003        Ultrasonic Calibration/Examination Sheet for RPV    October 22, 2009
Ultrasonic Calibration/Examination Sheet for RHR
              Meridonal Weld, ISI Number CH-101-104-C
Pipe to Pipe Weld , ISI Number EJ-04-F019
AWJ004        Ultrasonic Calibration/Examination Sheet for RPV    October 22, 2009
October 22, 2009
              Meridonal Weld, ISI Number CH-101-104-B
JEW015
ET 05-0014    Docket 50-482: 10 CFR 50.55a Request Number        September 28, 2005
Ultrasonic Calibration/Examination Sheet for  
              I3R-03 for the Third Ten-Year Interval Inservice
SI/HPCI Pipe to Elbow Weld, ISI Number EM-03-
              Inspection (ISI) Program - Request for Relief to
S015-B
              Allow Use of Alternate Requirements for Snubber
October 22, 2009  
              Inspection and Testing
M-12KJ04
ET 06-0010    Docket 50-482: Inservice Inspection Program Plan      March 2, 2006
Piping and Instrumentation Diagram Standby
              for the Third Ten-Year Interval and 10 CFR 50.55a
Diesel Generator B Lube Oil System
              Requests I3R-01, I3R-02, and I3R-04
13
                                  A-9                                Attachment 1
M-12KJ06
Piping and Instrumentation Diagram Standby
Diesel Generator B Lube Oil System
13
M-13EF08
Piping Isometric Essential Service Water- Diesel
Generator Bldg.
1
QCF 20-510-01
Ultrasonic Instrument Linearity Form
2
QCF-20-100-01
Contractor Certification Review
2
QCF-20-504-02
Ultrasonic Flaw Detection Data Sheet  
2
QCF-20-504-06
Ultrasonic Flaw Detection Calibration Data Sheet  
0
SAP-+PT-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-+PTUB-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-01-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-02-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-03-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-04-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0


    NUMBER                         TITLE                       REVISION / DATE
ET 06-0021  Docket No. 50-482: 10 CFR 50.55a Request I3R-         May 19. 2006
            05, Installation and Examination of Full Structural
A-12
            Weld Overlays for Repairing/Mitigating Pressurizer
            Nozzle-to-Safe End Dissimilar Metal Welds and
            Adjacent Safe End-to-Piping Stainless Steel Welds
ET 06-0042  Docket 50-482: Wolf Creek Nuclear Operating        September 27, 2006
            Corporations Response to the September 20,
Attachment 1
            2006 NRC Request for Additional Information
NUMBER  
            Regarding 10 CFR 50.55a Request I3R-05
TITLE  
ET 06-0043  Docket 50-482: Wolf Creek Nuclear Operating          October 5, 2006
REVISION / DATE  
            Corporations Response to NRC Request for
SAP-05-09
            Additional Information Regarding 10 CFR 50.55a
Steam Generator Eddy Current Inspection Multi-
            Request I3R-01
Frequency Eddy Current Parameters
ET 06-0044  Docket 50-482: Wolf Creek Nuclear Operating          October 2, 2006
0
            Corporations Revised Commitment Regarding 10
SAP-06-09
            CFR 50.55a Request I3R-05
Steam Generator Eddy Current Inspection Multi-
ET 06-0058  Docket No. 50-482: Wolf Creek Nuclear Operating December 20, 2006
Frequency Eddy Current Parameters
            Corporations Response to the Second NRC
0
            Request for Additional Information Regarding 10
SAP-07-09
            CFR 50.55a Request I3R-01
Steam Generator Eddy Current Inspection Multi-
ET 08-0044  Docket No. 50-482: 10 CFR 50.55a Request I3R-       September 16, 2008
Frequency Eddy Current Parameters
            06, Alternative to Examination Requirements of
0
            ASME Section XI for Class 1 Piping Welds
SAP-08-09
            Examined from the Inside of the Reactor Vessel
Steam Generator Eddy Current Inspection Multi-
ET 09-0016  Docket No. 50-482: Revision to Technical                June 2. 2009
Frequency Eddy Current Parameters
            Specifications 5.5.9, Steam Generator (SG)
0
            Program, and TS 5.6.10, Steam Generator Tube
SAP-09-09
            Inspection Report, for a Permanent Alternate
Steam Generator Eddy Current Inspection Multi-
            Repair Criterion
Frequency Eddy Current Parameters
ET 09-0021  Docket No. 50-482: Response to Request for           August 25, 2009
0
            Additional Information Related to License
SAP-10-09
            Amendment Request for a Permanent Alternate
Steam Generator Eddy Current Inspection Multi-
            Repair Criterion to Technical Specification 5.5.9,
Frequency Eddy Current Parameters
            Steam Generator (SG) Program
0
ET 09-0023  Docket No. 50-482: Response to Request for           September 3, 2009
SAP-11-09
            Additional Information Related to License
Steam Generator Eddy Current Inspection Multi-
            Amendment Request for a Permanent Alternate
Frequency Eddy Current Parameters
            Repair Criterion to Technical Specification 5.5.9,
0
            Steam Generator (SG) Program
SAP-12-09
                              A-10                                Attachment 1
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-BOB-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-DELTA-09
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SAP-GHENT-09  
Steam Generator Eddy Current Inspection Multi-
Frequency Eddy Current Parameters
0
SEL 04-038
Steam Generator Program
4
  SG-CDME-08-15
Wolf Creek RF16 Condition Monitoring
Assessment and Operational Assessment, April
2008
1
SG-CDME-09-1
Wolf Creek Steam Generator Secondary Side
Condition Monitoring and Operational Assessment
for Fuel Cycle and Refueling Outage 17
0
SG-SGMP-09-9
Steam Generator Degradation Assessment for  
Wolf Creek, RF17 Refueling Outage, October 2009  
0
WDI-LTR-
ENG-09-0016
Technical Justification of the Impact of Using
Tap/Demineralized Water for UT System
Calibration and Borated Reactor Cavity Water for  
RVISI UT Examinations.  
0


    NUMBER                          TITLE                      REVISION / DATE
ET 09-0024    Docket No. 50-482: Response to Request for        September 3, 2009
              Clarifications in Response to Application for
A-13
              Withholding Proprietary Information from Public
              Disclosure (TAC NO. ME1393)
ET 09-0025    Docket No. 50-482: Revision to Technical        September 15, 2009
              Specification (TS) 5.5.9, Steam Generator (SG)
              Program, and TS 5.6.10, Steam Generator Tube
Attachment 1
              Inspection Report
Section 1R12: Maintenance Effectiveness
I-ENG-023    Steam Generator Data Analysis Guidelines                  8
JEW014        Ultrasonic Calibration/Examination Sheet for RHR  October 22, 2009
MISCELLANEOUS
              Pipe to Pipe Weld , ISI Number EJ-04-F019
JEW015        Ultrasonic Calibration/Examination Sheet for      October 22, 2009
NUMBER
              SI/HPCI Pipe to Elbow Weld, ISI Number EM-03-
TITLE
              S015-B
REVISION /  
              Piping and Instrumentation Diagram Standby                13
DATE
M-12KJ04
EG-01
              Diesel Generator B Lube Oil System
Maintenance Rule Database - Component Cooling
              Piping and Instrumentation Diagram Standby                13
Water - Engineered Safety Features System Cooling
M-12KJ06
n/a
              Diesel Generator B Lube Oil System
EG-03  
              Piping Isometric Essential Service Water- Diesel          1
Maintenance Rule Database - Component Cooling
M-13EF08
Water System - RCP Thermal Barrier Cooling
              Generator Bldg.
n/a
QCF 20-510-01 Ultrasonic Instrument Linearity Form                      2
EG-07
QCF-20-100-01 Contractor Certification Review                          2
Maintenance Rule Database - Component Cooling
QCF-20-504-02 Ultrasonic Flaw Detection Data Sheet                      2
Water System - ESW Frazil Ice Prevention
QCF-20-504-06 Ultrasonic Flaw Detection Calibration Data Sheet          0
n/a
              Steam Generator Eddy Current Inspection Multi-           0
M-11EG02
SAP-+PT-09
System Flow Diagram Component Cooling Water
              Frequency Eddy Current Parameters
System
              Steam Generator Eddy Current Inspection Multi-           0
2
SAP-+PTUB-09
M-762-001-02
              Frequency Eddy Current Parameters
Nuclear Instrumentation System Source Range N-31
              Steam Generator Eddy Current Inspection Multi-           0
Functional Block Diagram
SAP-01-09
7
              Frequency Eddy Current Parameters
PIR 2004-1625
              Steam Generator Eddy Current Inspection Multi-            0
Two Source Range Channels are Required to
SAP-02-09
Perform Core Alterations During a Refueling Outage
              Frequency Eddy Current Parameters
June 22,
              Steam Generator Eddy Current Inspection Multi-             0
2004
SAP-03-09
SE-01  
              Frequency Eddy Current Parameters
Maintenance Rule Database - Source Range
              Steam Generator Eddy Current Inspection Multi-            0
Nuclear Instrumentation
SAP-04-09
n/a
              Frequency Eddy Current Parameters
SE-02  
                                A-11                              Attachment 1
Maintenance Rule Database - Intermediate Range
Nuclear Instrumentation
n/a
OFN PK-029
Loss of Non-Vital 125 VDC Bus PK01, PK02, PK03,
PK4, and Annunciators
15
STS IC-232
Channel Operational Test Nuclear Instrumentation
System Source Range N-32 Protection Set II
15
AI 28A-023
Evaluation of Maintenance Rule Functional Failure
1
AP 23M-001
WCGS Maintenance Rule Program
7
EDI 23M-050
Establishing Performance Criteria for Structures,
Systems and Components with the Scope of the
Maintenance Rule
3
WCN-7328
Report on ECAD Testing at Wolf Creek Generating
Station
October 28,
2009
WR 5047865
Functional Failure Determination (EDI 23M-050)
April 24,
2005
Maintenance Rule Expert Panel Meeting Minutes
February 18
, 1999


    NUMBER                           TITLE                   REVISION / DATE
              Steam Generator Eddy Current Inspection Multi-          0
SAP-05-09
A-14
              Frequency Eddy Current Parameters
              Steam Generator Eddy Current Inspection Multi-          0
SAP-06-09
              Frequency Eddy Current Parameters
              Steam Generator Eddy Current Inspection Multi-          0
Attachment 1
SAP-07-09
NUMBER  
              Frequency Eddy Current Parameters
TITLE  
              Steam Generator Eddy Current Inspection Multi-          0
REVISION /  
SAP-08-09
DATE  
              Frequency Eddy Current Parameters
              Steam Generator Eddy Current Inspection Multi-          0
Maintenance Rule Expert Panel Meeting Minutes
SAP-09-09
April 10,
              Frequency Eddy Current Parameters
2000
              Steam Generator Eddy Current Inspection Multi-         0
SAP-10-09
Maintenance Rule Expert Panel Meeting Minutes
              Frequency Eddy Current Parameters
April 24,
              Steam Generator Eddy Current Inspection Multi-         0
2000
SAP-11-09
              Frequency Eddy Current Parameters
WORK ORDERS
              Steam Generator Eddy Current Inspection Multi-         0
SAP-12-09
NUMBER
              Frequency Eddy Current Parameters
TITLE
              Steam Generator Eddy Current Inspection Multi-         0
REVISION /
SAP-BOB-09
DATE
              Frequency Eddy Current Parameters
WO 07-293925-000
              Steam Generator Eddy Current Inspection Multi-          0
Replace Electrolytic Capacitors or Replace Power
SAP-DELTA-09
Supply NIS Source Range Hi Voltage Power Supply
              Frequency Eddy Current Parameters
March 31,
              Steam Generator Eddy Current Inspection Multi-          0
2008
SAP-GHENT-09
WO 08-302634-000
              Frequency Eddy Current Parameters
Perform STN IC-031 Source Range N-31 High Flux
SEL 04-038    Steam Generator Program                                4
at Shutdown Alarm Calibration
              Wolf Creek RF16 Condition Monitoring                    1
January 12,
SG-CDME-08-15 Assessment and Operational Assessment, April
2008
              2008
WO 08-302635-000
              Wolf Creek Steam Generator Secondary Side              0
Perform STN IC-032 Source Range N-32 High Flux
SG-CDME-09-1  Condition Monitoring and Operational Assessment
at Shutdown Alarm Calibration
              for Fuel Cycle and Refueling Outage 17
January 12,
              Steam Generator Degradation Assessment for              0
2008
SG-SGMP-09-9
WO 08-305403-000
              Wolf Creek, RF17 Refueling Outage, October 2009
Refuel 16 Perform STN IC-031 Source Range N-31
              Technical Justification of the Impact of Using          0
High Flux at Shutdown Alarm Calibration
WDI-LTR-       Tap/Demineralized Water for UT System
April 11,
ENG-09-0016    Calibration and Borated Reactor Cavity Water for
2008
              RVISI UT Examinations.
WO 08-305404-000
                                A-12                            Attachment 1
Refuel 16 Perform STN IC-032 Source Range N-32
High Flux at Shutdown Alarm Calibration
April 11,
2008
WO 08-310573-000
Replace Electrolytic Capacitors or Replace Power
Supply
August 13,
2009
WO 09-314187-000
Retorque CCW Pump to Motor Coupling Bolts
February
12, 2009
WO 09-316487-000
Troubleshoot IR SE NI-36 to Determine Why it Hung
Up Following RX Trip on 4/28 and Repair as
Necessary
April 28,  
2009
WO 09-318691-000
Troubleshoot CCW Return from RCP Thermal
Barrier High Flow Setpoint
September
22, 2009
WO 09-320716-000
Refuel 17.  Perform Detector and Cable Integrity
Checks for SR, IR, and PR NIS Channels
October 10,
2009
WO 09-320874-000
Troubleshoot Source Range Channel 31 to
Determine Why it Failed After it was Energized
October 10,
2009
WO 09-320874-001
Replace High Voltage Power Supply (NQ101) in
N-31 Source Range during partial STS IC-431
October 10,  
2009  
WO 09-320874-005
Replace R150 in N-31
October 10,
2009


Section 1R12: Maintenance Effectiveness
MISCELLANEOUS
      NUMBER                                 TITLE                         REVISION /
A-15
                                                                              DATE
EG-01                Maintenance Rule Database - Component Cooling            n/a
                      Water - Engineered Safety Features System Cooling
  EG-03                Maintenance Rule Database - Component Cooling            n/a
                      Water System - RCP Thermal Barrier Cooling
Attachment 1
EG-07                Maintenance Rule Database - Component Cooling            n/a
NUMBER  
                      Water System - ESW Frazil Ice Prevention
TITLE  
  M-11EG02              System Flow Diagram Component Cooling Water                2
REVISION /  
                      System
DATE  
  M-762-001-02          Nuclear Instrumentation System Source Range N-31          7
WR 09-076482
                      Functional Block Diagram
During the Performance of STS IC-432 the Two-Phi
  PIR 2004-1625        Two Source Range Channels are Required to              June 22,
Meter Failed to Alarm Annunciator
                      Perform Core Alterations During a Refueling Outage      2004
October 24,
  SE-01                Maintenance Rule Database - Source Range                  n/a
2009
                      Nuclear Instrumentation
  SE-02                Maintenance Rule Database - Intermediate Range            n/a
WORK ORDERS
                      Nuclear Instrumentation
   
OFN PK-029            Loss of Non-Vital 125 VDC Bus PK01, PK02, PK03,          15
WO 05-270366-000
                      PK4, and Annunciators
WO 05-270366-006
STS IC-232            Channel Operational Test Nuclear Instrumentation          15
WO 06-288260-000
                      System Source Range N-32 Protection Set II
AI 28A-023            Evaluation of Maintenance Rule Functional Failure          1
CONDITION REPORTS
AP 23M-001           WCGS Maintenance Rule Program                             7
   
EDI 23M-050          Establishing Performance Criteria for Structures,          3
CR 20052
                      Systems and Components with the Scope of the
CR 01880
                      Maintenance Rule
   
WCN-7328              Report on ECAD Testing at Wolf Creek Generating       October 28,
                      Station                                                  2009
   
WR 5047865            Functional Failure Determination (EDI 23M-050)         April 24,
Section 1R13:  Maintenance Risk Assessment and Emergent Work Controls
                                                                                2005
   
                      Maintenance Rule Expert Panel Meeting Minutes        February 18
MISCELLANEOUS
                                                                              , 1999
   
                                    A-13                                Attachment 1
NUMBER
TITLE
REVISION /  
DATE
AP 22B-001
Outage Risk Management
11
AP 22C-003
Operational Risk Assessment Program
14A
AP 23M-001  
WCGS Maintenance Rule Program  
7  
APF 22B-001-02
Daily Shutdown Risk Assessments for RFO 17
8
AI-07A-008
Lake Water Chemical Treatment Program
16
AP 23L-001
Lake Water Systems Corrosion and Fouling
Mitigation Program
2
SYS EF-300
ESW/Service Water Macrofoul Treatment
22
WCEM-06-005
Zebra Mussel Monitoring - 2008 Report and 2009
Plan
9
RNT 745679/0
Assessment of the Potential Impact of Zebra
Mussels on the Wolf Creek Power Plant and
Recommendations for Control 
July 20, 2009
900030
Customer Assembly Neutron Flux Monitor System,
SNUPPS Generating Stations, Callaway 1 (Union
Elec Co) and Wolf Creek (Kansas Gas & Electric)  
F
CCP 013096
Instrument Setpoints for RCP Thermal Barrier
Isolation and EGHV0062 Valves
1  


      NUMBER                            TITLE                        REVISION /
                                                                          DATE
                  Maintenance Rule Expert Panel Meeting Minutes          April 10,
A-16
                                                                          2000
                  Maintenance Rule Expert Panel Meeting Minutes          April 24,
                                                                          2000
WORK ORDERS
      NUMBER                             TITLE                       REVISION /
Attachment 1
                                                                          DATE
NUMBER  
WO 07-293925-000 Replace Electrolytic Capacitors or Replace Power      March 31,
TITLE  
                  Supply NIS Source Range Hi Voltage Power Supply        2008
REVISION /  
  WO 08-302634-000 Perform STN IC-031 Source Range N-31 High Flux      January 12,
DATE  
                  at Shutdown Alarm Calibration                          2008
EQDP-ESE-47A
WO 08-302635-000 Perform STN IC-032 Source Range N-32 High Flux      January 12,
Boron Dilution Fix:  Source/Intermediate Range  
                  at Shutdown Alarm Calibration                          2008
Neutron Detector
WO 08-305403-000 Refuel 16 Perform STN IC-031 Source Range N-31        April 11,
  0
                  High Flux at Shutdown Alarm Calibration                2008
M-762-00018-W03
WO 08-305404-000 Refuel 16 Perform STN IC-032 Source Range N-32        April 11,
Source and Intermediate Range Detector Assembly
                  High Flux at Shutdown Alarm Calibration                2008
August 19,  
WO 08-310573-000 Replace Electrolytic Capacitors or Replace Power    August 13,
1988
                  Supply                                                  2009
NY-10042
WO 09-314187-000 Retorque CCW Pump to Motor Coupling Bolts            February
Class 1E Qualified Proportional Counter and
                                                                        12, 2009
Compensated Ionization Chamber Insulated
  WO 09-316487-000 Troubleshoot IR SE NI-36 to Determine Why it Hung      April 28,
Assembly
                  Up Following RX Trip on 4/28 and Repair as              2009
September
                  Necessary
1990
  WO 09-318691-000 Troubleshoot CCW Return from RCP Thermal            September
NY-10044
                  Barrier High Flow Setpoint                            22, 2009
Qualified* Class 1E BF3 Proportional Counter
  WO 09-320716-000 Refuel 17. Perform Detector and Cable Integrity      October 10,
Assembly
                  Checks for SR, IR, and PR NIS Channels                  2009
September
WO 09-320874-000 Troubleshoot Source Range Channel 31 to              October 10,
1990
                  Determine Why it Failed After it was Energized          2009
OE SE-09-008
WO 09-320874-001 Replace High Voltage Power Supply (NQ101) in        October 10,
Source Range Nuclear Instrument SEN0031
                  N-31 Source Range during partial STS IC-431            2009
00
WO 09-320874-005 Replace R150 in N-31                                October 10,
OE SE-09-011
                                                                          2009
Source Range Nuclear Instrument SEN0032
                                A-14                                Attachment 1
00
USAR 9.4.6
Containment HVAC
19
STS AE-205
Feedwater System Inservice Valve Test
November 120
09  
LCO 3.0.4
Wolf Creek Technical Specifications
November 182
009
APF 22C-003-01
Operational Risk Assessment
November 172
009
n/a
Wolf Creek Operations Logs: Control Room Log
n/a
n/a
Wolf Creek Operations Logs: Equipment Out of
Service Log
n/a
n/a
Technical Specification LCO 3.0.4 Mode Change
Review Form - TDAFWP Inoperable
November 17,  
2009  
   
CONDITION REPORTS
NUMBER
TITLE
REVISION /
DATE
CR 19528
SOER 09-1: Shutdown Safety
September 1,  
2009  
CR 21286
ESW Self Cleaning Strainer Tubes Retain Debris
October 28,  
2009  
CR 19282
Source Range N31 Indication During Loss of Cavity
Cooling
August 20,  
2009  


      NUMBER                                 TITLE                       REVISION /
                                                                            DATE
WR 09-076482          During the Performance of STS IC-432 the Two-Phi    October 24,
A-17
                      Meter Failed to Alarm Annunciator                      2009
WORK ORDERS
  WO 05-270366-000           WO 05-270366-006              WO 06-288260-000
CONDITION REPORTS
CR 20052            CR 01880
Attachment 1
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
NUMBER  
MISCELLANEOUS
TITLE  
      NUMBER                                 TITLE                         REVISION /
REVISION /  
                                                                              DATE
DATE  
AP 22B-001            Outage Risk Management                                    11
CR 20208
AP 22C-003            Operational Risk Assessment Program                      14A
Source Range Detector Operability Question
AP 23M-001            WCGS Maintenance Rule Program                              7
September 30,
APF 22B-001-02        Daily Shutdown Risk Assessments for RFO 17                8
2009
AI-07A-008           Lake Water Chemical Treatment Program                     16
CR 20325
AP 23L-001           Lake Water Systems Corrosion and Fouling                   2
Effect on Cavity Components with Loss of Cavity
                      Mitigation Program
Cooling
SYS EF-300           ESW/Service Water Macrofoul Treatment                     22
October 6,  
WCEM-06-005           Zebra Mussel Monitoring - 2008 Report and 2009             9
2009
                      Plan
CR 21906
RNT 745679/0          Assessment of the Potential Impact of Zebra        July 20, 2009
T/S Log Entries Related to Entering Mode 3 with
                      Mussels on the Wolf Creek Power Plant and
TDAFWP OOS
                      Recommendations for Control
November 19,
900030                Customer Assembly Neutron Flux Monitor System,            F
2009
                      SNUPPS Generating Stations, Callaway 1 (Union
CR 21926
                      Elec Co) and Wolf Creek (Kansas Gas & Electric)
Inconsistent Directions for Protected Train Signs in
CCP 013096            Instrument Setpoints for RCP Thermal Barrier              1
Mode 3
                      Isolation and EGHV0062 Valves
November 19,
                                    A-15                              Attachment 1
2009
CR 21286
ESW Self Cleaning Strainer Tubes Retain Debris
October 28,
2009  
WORK ORDERS  
   
NUMBER
TITLE
REVISION /
DATE
WO 09-322198-000  
Create a RM/Repetitive Task to Open the ESW Self
Cleaning Strainers and Clean the Porous Strainer
Tubes
November 12,
2009
WO 09-319411-001
Source Range NI 31 Indication is Trending Up. 
Evaluate Condition to Determine Cause
August 22,
2009
Section 1R15: Operability Evaluations
MISCELLANEOUS  
NUMBER  
TITLE  
REVISION /  
DATE  
OE SE-09-008
Source Range Nuclear Instrument SEN0031
00
AI-07A-008  
Lake Water Chemical Treatment Program  
16  
AP 23L-001  
Lake Water Systems Corrosion and Fouling  
Mitigation Program  
2
AP 28-001
Operability Evaluations
17
AP 26C-004
Technical Specification Operability
January 13,
2010
SYS EF-300  
ESW/Service Water Macrofoul Treatment  
22  
WCEM-06-005  
Zebra Mussel Monitoring - 2008 Report and 2009  
Plan  
9


      NUMBER                             TITLE                         REVISION /
                                                                          DATE
  EQDP-ESE-47A     Boron Dilution Fix: Source/Intermediate Range               0
A-18
                  Neutron Detector
  M-762-00018-W03 Source and Intermediate Range Detector Assembly       August 19,
                                                                          1988
NY-10042         Class 1E Qualified Proportional Counter and           September
                  Compensated Ionization Chamber Insulated                 1990
Attachment 1
                  Assembly
NUMBER  
NY-10044         Qualified* Class 1E BF3 Proportional Counter         September
TITLE  
                  Assembly                                                1990
REVISION /  
OE SE-09-008     Source Range Nuclear Instrument SEN0031                   00
DATE  
OE SE-09-011     Source Range Nuclear Instrument SEN0032                   00
RNT 745679/0
USAR 9.4.6       Containment HVAC                                           19
Assessment of the Potential Impact of Zebra
STS AE-205       Feedwater System Inservice Valve Test               November 120
Mussels on the Wolf Creek Power Plant and
                                                                            09
Recommendations for Control 
LCO 3.0.4        Wolf Creek Technical Specifications                November 182
July 20,
                                                                            009
2009
APF 22C-003-01  Operational Risk Assessment                        November 172
900030
                                                                            009
Customer Assembly Neutron Flux Monitor System,
n/a             Wolf Creek Operations Logs: Control Room Log             n/a
SNUPPS Generating Stations, Callaway 1 (Union
n/a             Wolf Creek Operations Logs: Equipment Out of             n/a
Elec Co) and Wolf Creek (Kansas Gas & Electric)
                  Service Log
F
n/a             Technical Specification LCO 3.0.4 Mode Change       November 17,
CCP 013096
                  Review Form - TDAFWP Inoperable                         2009
Instrument Setpoints for RCP Thermal Barrier
CONDITION REPORTS
Isolation and EGHV0062 Valves
      NUMBER                            TITLE                        REVISION /
1
                                                                          DATE
EQDP-ESE-47A  
CR 19528        SOER 09-1: Shutdown Safety                          September 1,
Boron Dilution Fix: Source/Intermediate Range  
                                                                          2009
Neutron Detector  
CR 21286        ESW Self Cleaning Strainer Tubes Retain Debris        October 28,
  0
                                                                          2009
M-762-00018-W03  
CR 19282        Source Range N31 Indication During Loss of Cavity    August 20,
Source and Intermediate Range Detector Assembly  
                  Cooling                                                  2009
August 19,  
                                A-16                                Attachment 1
1988  
NY-10042  
Class 1E Qualified Proportional Counter and  
Compensated Ionization Chamber Insulated  
Assembly  
September
1990
NY-10044  
Qualified* Class 1E BF3 Proportional Counter  
Assembly
September  
1990  
OE SE-09-008  
Source Range Nuclear Instrument SEN0031  
00  
OE SE-09-011  
Source Range Nuclear Instrument SEN0032  
00  
USAR 9.4.6  
Containment HVAC  
19  
STS AE-205  
Feedwater System Inservice Valve Test  
November  
9, 2009
n/a  
Wolf Creek Operations Logs: Control Room Log  
n/a  
n/a  
Wolf Creek Operations Logs: Equipment Out of  
Service Log
n/a  
LCO 3.0.4
Wolf Creek Technical Specifications
November
18, 2009
n/a  
Technical Specification LCO 3.0.4 Mode Change  
Review Form - TDAFWP Inoperable  
November
17, 2009  
APF 22C-003-01
Operational Risk Assessment
November
17, 2009
M-089-K027-06
Byron Jackson Report DC-1104
3
EF-S-043
Determine the Stress in the Essential Service Water
Pump (PEF01A) column housing using specified
maximum deflection
0


      NUMBER                                    TITLE                            REVISION /
                                                                                    DATE
  CR 20208               Source Range Detector Operability Question            September 30,
A-19
                                                                                    2009
CR 20325                Effect on Cavity Components with Loss of Cavity          October 6,
                        Cooling                                                    2009
CR 21906                T/S Log Entries Related to Entering Mode 3 with        November 19,
   
                        TDAFWP OOS                                                  2009
Attachment 1
CR 21926               Inconsistent Directions for Protected Train Signs in    November 19,
CONDITION REPORTS
                        Mode 3                                                      2009
CR 19282
  CR 21286                ESW Self Cleaning Strainer Tubes Retain Debris          October 28,
CR 20208  
                                                                                    2009
CR 20325
WORK ORDERS
CR 21906
      NUMBER                                   TITLE                           REVISION /
CR 22798
                                                                                    DATE
CR 21574
WO 09-322198-000        Create a RM/Repetitive Task to Open the ESW Self        November 12,
CR 21400
                        Cleaning Strainers and Clean the Porous Strainer            2009
CR 21572
                        Tubes
CR 21926  
WO 09-319411-001       Source Range NI 31 Indication is Trending Up.             August 22,
                        Evaluate Condition to Determine Cause                       2009
   
Section 1R15: Operability Evaluations
WORK ORDERS  
MISCELLANEOUS
      NUMBER                                   TITLE                         REVISION /
NUMBER  
                                                                                    DATE
TITLE  
OE SE-09-008            Source Range Nuclear Instrument SEN0031                    00
REVISION /  
AI-07A-008              Lake Water Chemical Treatment Program                      16
DATE  
AP 23L-001              Lake Water Systems Corrosion and Fouling                    2
WO 09-319411-001  
                        Mitigation Program
Source Range NI 31 Indication is Trending Up.
AP 28-001              Operability Evaluations                                    17
Evaluate Condition to Determine Cause  
AP 26C-004              Technical Specification Operability                    January 13,
August 22,
                                                                                    2010
2009  
SYS EF-300              ESW/Service Water Macrofoul Treatment                      22
WO 09-322198-000
WCEM-06-005            Zebra Mussel Monitoring - 2008 Report and 2009              9
                        Plan
                                      A-17                                  Attachment 1
Section 1R18: Plant Modifications
NUMBER  
TITLE  
REVISION  
AP 05-010
Design Drawings
6
AP 05D-001
Calculations
12
AP 05A-001
Design Inputs
1
AP 05-002
Dispositions and Change Packages
8
AP 05-005
Design, Implementation & Configuration of
Modifications
13
WCRE-01
Total Plant Setpoint Document
32
CCP 013096
Instrument Setpoints for RCP Thermal Barrier
Isolation and EGHV0062 Valves
01
AP 05-013
Review of Vendor Technical Documents
7A
NP 92-0996
Interoffice Correspondence from C. R. Morris, CCW
Low Transient (PMR 03580) Meeting
5/21/92
EG-M-016
Time Delay for Isolation of CCW High Flow to RCP
Thermal Barriers
1
M-738-0032-02
Functional Requirements and Design Criteria
Standard Single and Twin Units 212, 312, 412 Plants
Component Cooling System
3
CONDITION REPORT
CR 16243


      NUMBER                            TITLE                        REVISION /
                                                                          DATE
RNT 745679/0    Assessment of the Potential Impact of Zebra            July 20,
A-20  
                Mussels on the Wolf Creek Power Plant and                2009
                Recommendations for Control
900030          Customer Assembly Neutron Flux Monitor System,              F
                SNUPPS Generating Stations, Callaway 1 (Union
                Elec Co) and Wolf Creek (Kansas Gas & Electric)
Attachment 1  
CCP 013096      Instrument Setpoints for RCP Thermal Barrier                1
Section 1R19:  Postmaintenance Testing
                Isolation and EGHV0062 Valves
EQDP-ESE-47A    Boron Dilution Fix: Source/Intermediate Range                0
NUMBER
                Neutron Detector
TITLE
M-762-00018-W03 Source and Intermediate Range Detector Assembly        August 19,
REVISION
                                                                          1988
STN EF-201
NY-10042        Class 1E Qualified Proportional Counter and            September
ESW System Valve Test
                Compensated Ionization Chamber Insulated                  1990
2A
                Assembly
AP 16E-002
NY-10044        Qualified* Class 1E BF3 Proportional Counter          September
Post Maintenance Testing Development
                Assembly                                                  1990
8
OE SE-09-008    Source Range Nuclear Instrument SEN0031                    00
AP 23D-001
OE SE-09-011    Source Range Nuclear Instrument SEN0032                      00
Motor Operated Valve Program
USAR 9.4.6      Containment HVAC                                            19
2
STS AE-205      Feedwater System Inservice Valve Test                  November
STS IC-608A
                                                                        9, 2009
Slave Relay Test K608A Train A Safety Injection
n/a            Wolf Creek Operations Logs: Control Room Log                n/a
18
n/a            Wolf Creek Operations Logs: Equipment Out of               n/a
                Service Log
CONDITION REPORT
LCO 3.0.4      Wolf Creek Technical Specifications                    November
                                                                        18, 2009
CR 19670
n/a            Technical Specification LCO 3.0.4 Mode Change          November
                Review Form - TDAFWP Inoperable                        17, 2009
WORK ORDERS
APF 22C-003-01  Operational Risk Assessment                            November
                                                                        17, 2009
06-291566-001
M-089-K027-06  Byron Jackson Report DC-1104                                3
06-291566-012
EF-S-043        Determine the Stress in the Essential Service Water          0
09-316118-001
                Pump (PEF01A) column housing using specified
                maximum deflection
                              A-18                                  Attachment 1
Section 1R20:  Refueling and Other Outage Activities
NUMBER
TITLE
REVISION
WCRE-16
Inservice Inspection Program Plan Wolf Creek
Generating Station Interval 3
4  
WCRE-23
Inservice Inspection Classification Basis Document
Wolf Creek Generating Station Interval 3
3/24/09
SYS BB-112
Vacuum Fill of the RCS
27
GEN 00-008
Reduced Inventory Operations
19
GEN 00-009
Refueling
23
GEN 00-003  
Hot Standby to Minimum Load
73
SYS BB-215
RCS Drain Down with Fuel in Reactor
23A
STS RE-002
Determination of Estimated Critical Position
18
APF 19C-002-01
Wolf Creek Generating Station Fuel Transfer
Authorization
0
APF 22B-001-02
Daily Shutdown Risk Assessment
8
RWP 092602
Radiation Work Permit
1
RWP 092602
ALARA Review Package
7
RWP 091102
Radiation Work Permit
0  
RWP 091102
ALARA Review Package
7


CONDITION REPORTS
  CR 19282        CR 20208          CR 20325          CR 21906          CR 22798
CR 21574        CR 21400          CR 21572          CR 21926
A-21
WORK ORDERS
      NUMBER                                  TITLE                        REVISION /
                                                                                DATE
WO 09-319411-001      Source Range NI 31 Indication is Trending Up.          August 22,
                        Evaluate Condition to Determine Cause                    2009
Attachment 1
WO 09-322198-000
NUMBER
Section 1R18: Plant Modifications
TITLE
      NUMBER                                  TITLE                        REVISION
REVISION
  AP 05-010              Design Drawings                                            6
RWP 091102
  AP 05D-001            Calculations                                              12
Radiation Work Permit
  AP 05A-001            Design Inputs                                              1
0
  AP 05-002              Dispositions and Change Packages                            8
EID-0003
  AP 05-005              Design, Implementation & Configuration of                  13
Refuel Level Indications
                        Modifications
2
WCRE-01                Total Plant Setpoint Document                              32
M-19BG24
CCP 013096            Instrument Setpoints for RCP Thermal Barrier              01
Hanger Location DWG. Small Pipe CVCS Auxiliary
                        Isolation and EGHV0062 Valves
Spray Reactor Building
AP 05-013              Review of Vendor Technical Documents                      7A
7
NP 92-0996            Interoffice Correspondence from C. R. Morris, CCW      5/21/92
M-15BG21
                        Low Transient (PMR 03580) Meeting
Hanger Location DWG. Small Pipe CVCS - Normal
EG-M-016              Time Delay for Isolation of CCW High Flow to RCP            1
& Alternate Charging Reactor Building
                        Thermal Barriers
12
M-738-0032-02          Functional Requirements and Design Criteria                3
M-12BG01
                        Standard Single and Twin Units 212, 312, 412 Plants
Piping & Instrumentation Diagram Chemical and
                        Component Cooling System
Volume Control System
CONDITION REPORT
14
CR 16243
M-12BB02
                                      A-19                                Attachment 1
Piping & Instrumentation Diagram Reactor Coolant
System
16
n/a
Investigation into the Extent of Condition Related to
Linear Indications Discovered on Pressurizer
Auxiliary Spray Line at Wolf Creek Generating
Station
November 4,
2009
CONDITION REPORTS  
   
CR 20528
CR 20628
CR 21366
CR 21387
CR 21719
CR 20622
CR 20893
WORK ORDERS  
WO 09-321462-015
WO 08-303356-004
WO 09-321902-001
WO 08-303356-001
   
   
Section 1R22: Surveillance Testing
   
MISCELLANEOUS
   
NUMBER
TITLE
REVISION
STS AL-210A
MDAFW Pump A inservice check valve test
10
WCOP 02
Inservice Testing Program for Pumps and Valves  
14
AP 29B-002
ASME code testing of pumps and valves
7
AP 29B-003
Surveillance Testing
10
AP 29B-001
IST Basis Document
3


Section 1R19: Postmaintenance Testing
      NUMBER                                    TITLE                        REVISION
STN EF-201            ESW System Valve Test                                     2A
A-22
  AP 16E-002             Post Maintenance Testing Development                      8
  AP 23D-001             Motor Operated Valve Program                               2
  STS IC-608A            Slave Relay Test K608A Train A Safety Injection          18
CONDITION REPORT
CR 19670
Attachment 1
WORK ORDERS
STS AL-212
06-291566-001        06-291566-012          09-316118-001
MD AFP Comprehensive Pump Testing Flow Path
Section 1R20: Refueling and Other Outage Activities
Verification & Check Valve Testing
      NUMBER                                    TITLE                          REVISION
14
  WCRE-16                Inservice Inspection Program Plan Wolf Creek              4
AP 29A-004
                        Generating Station Interval 3
ASME Section XI System Pressure Testing  
  WCRE-23                Inservice Inspection Classification Basis Document      3/24/09
7
                        Wolf Creek Generating Station Interval 3
QCP 20-520
SYS BB-112            Vacuum Fill of the RCS                                      27
Pressure Test Examination
GEN 00-008            Reduced Inventory Operations                                19
8A
GEN 00-009            Refueling                                                  23
STS PE-007
  GEN 00-003            Hot Standby to Minimum Load                                73
Periodic Verification of Motor Operated Valves
  SYS BB-215            RCS Drain Down with Fuel in Reactor                        23A
   
  STS RE-002            Determination of Estimated Critical Position                18
3
  APF 19C-002-01          Wolf Creek Generating Station Fuel Transfer                0
AI 23D-002  
                        Authorization
MOV Calculation Guidelines  
APF 22B-001-02        Daily Shutdown Risk Assessment                              8
2
RWP 092602            Radiation Work Permit                                      1
AI 23D-003
  RWP 092602            ALARA Review Package                                        7
MOV Trending and Periodic Verification Program
  RWP 091102            Radiation Work Permit                                      0
1
  RWP 091102            ALARA Review Package                                        7
AP 29E-001  
                                      A-20                                Attachment 1
Program Plan for Containment Leakage
Measurement  
12
NEI 94-01
NEI Guideline for Implementing the Performance
Based Guideline of Appendix J
NEI 94-01
M-12AL01
Piping and Instrumentation Drawing Auxiliary
Feedwater
10
M-12AE01
Piping and Instrumentation Drawing Feedwater
37
M-12EF01
Piping and Instrumentation Drawing Essential
Service Water
21
M-12EF02
Piping and Instrumentation Drawing Essential
Service Water
25
M-724-00784
EJHV8811A/B Pressure Locking Bypass
W02
M-724-00696
Motor Operated Gate Valve
W06
M-12EJ01
Piping and Instrumentation Drawing Residual Heat
Removal System
43
   
CONDITION REPORTS
   
CR 1994-0881
CR 1998-0422
CR 2001-2237
CR 2005-1899
CR 2005-3545
CR 20723
CR 21308
CR 21343
   
   
   
WORK ORDERS
   
WO 05-278104-012
WO 09-321637-000
WO 09-321637-002
WO 09-321637-001
   
   
   


      NUMBER                                    TITLE                            REVISION
  RWP 091102              Radiation Work Permit                                          0
   
  EID-0003                Refuel Level Indications                                      2
A-23
  M-19BG24                Hanger Location DWG. Small Pipe CVCS Auxiliary                7
   
                        Spray Reactor Building
   
  M-15BG21                Hanger Location DWG. Small Pipe CVCS - Normal                12
                        & Alternate Charging Reactor Building
   
  M-12BG01                Piping & Instrumentation Diagram Chemical and                14
Attachment 1
                        Volume Control System
Section 2OS1:  Access Controls to Radiologically Significant Areas
  M-12BB02                Piping & Instrumentation Diagram Reactor Coolant              16
   
                        System
CORRECTIVE ACTION DOCUMENTS
n/a                    Investigation into the Extent of Condition Related to    November 4,
   
                        Linear Indications Discovered on Pressurizer                2009
20878
                        Auxiliary Spray Line at Wolf Creek Generating
15485
                        Station
14874
CONDITION REPORTS
19405
  CR 20528        CR 20628            CR 21366            CR 21387            CR 21719
19409
  CR 20622        CR 20893
21004
WORK ORDERS
20973
  WO 09-321462-015              WO 08-303356-004                WO 09-321902-001
20987
WO 08-303356-001
10196
Section 1R22: Surveillance Testing
9627
MISCELLANEOUS
2008-1576
      NUMBER                                     TITLE                           REVISION
21029
STS AL-210A            MDAFW Pump A inservice check valve test                      10
20976
WCOP 02                Inservice Testing Program for Pumps and Valves              14
5633
AP 29B-002              ASME code testing of pumps and valves                        7
   
AP 29B-003              Surveillance Testing                                        10
   
  AP 29B-001              IST Basis Document                                            3
PROCEDURES
                                        A-21                                    Attachment 1
   
NUMBER
TITLE
REVISION
AP 25A-700
Use of Temporary Shielding or Locked High Radiation Areas
and Very High Radiation Area Barricades
10
RPP 02-105
RWP
33
AP 22-01
Conduct of Pre-Job and Post-Job Briefs
9A
AP 25A-200
Access to Locked High or Very High Radiation Areas
20
SEC 01-206
High Security Key Control and Issue
32
AP 25B-200
Radiography Guidelines
12
RADIATION WORK PERMITS
93021
9220
92602
93230
Section 4OA2: Identification and Resolution of Problems
MISCELLANEOUS  
NUMBER  
TITLE  
REVISION  
SYS AF-200
High Pressure Heater Operations
8
AP 21-001
Conduct of Operations
43
AP 19E-002
Reactivity Management Program
13
CONDITION REPORTS
   
CR 18034
CR 04293
CR 2001-2255


  STS AL-212            MD AFP Comprehensive Pump Testing Flow Path              14
   
                      Verification & Check Valve Testing
  AP 29A-004            ASME Section XI System Pressure Testing                  7
A-24
  QCP 20-520            Pressure Test Examination                                8A
  STS PE-007            Periodic Verification of Motor Operated Valves            3
   
  AI 23D-002            MOV Calculation Guidelines                                2
   
  AI 23D-003            MOV Trending and Periodic Verification Program            1
   
  AP 29E-001            Program Plan for Containment Leakage                    12
Attachment 1
                      Measurement
   
  NEI 94-01            NEI Guideline for Implementing the Performance      NEI 94-01
Section 40A5: Other Activities (TI-172 Dissimilar Metal Welds)
                      Based Guideline of Appendix J
   
M-12AL01              Piping and Instrumentation Drawing Auxiliary            10
MISCELLANEOUS
                      Feedwater
   
M-12AE01              Piping and Instrumentation Drawing Feedwater            37
NUMBER
M-12EF01              Piping and Instrumentation Drawing Essential            21
TITLE
                      Service Water
REVISION
M-12EF02              Piping and Instrumentation Drawing Essential            25
UT-95
                      Service Water
Ultrasonic Examination of Austenitic Piping Welds
M-724-00784          EJHV8811A/B Pressure Locking Bypass                    W02
3
M-724-00696          Motor Operated Gate Valve                              W06
WCRE-24
M-12EJ01              Piping and Instrumentation Drawing Residual Heat        43
WESDYNE Year 2009 Reactor Vessel Nozzle Safe-
                      Removal System
end Examinations Program Plan
CONDITION REPORTS
0
CR 1994-0881    CR 1998-0422      CR 2001-2237      CR 2005-1899    CR 2005-3545
WDI-CAL-102
  CR 20723        CR 21308          CR 21343
Calibration Inspection Procedure for PCI Eddy
WORK ORDERS
Current Card
  WO 05-278104-012            WO 09-321637-000                WO 09-321637-002
1
  WO 09-321637-001
WDI-EQPT-1021
                                      A-22                                Attachment 1
Installation and Removal of the WESDYNE Nozzle
Scanner (SQUID)
4
WDI-EQPT-1022
Reactor Vessel Nozzle Scanner Setup and Checkout
2
WDI-STD-146
ET Examination of Reactor Vessel Pipe Welds Inside
Surface
9
   
   
   


Section 2OS1: Access Controls to Radiologically Significant Areas
CORRECTIVE ACTION DOCUMENTS
20878          15485                14874            19405          19409
A2-1
21004          20973                20987            10196          9627
2008-1576      21029                20976            5633
PROCEDURES
    NUMBER                                  TITLE                          REVISION
AP 25A-700      Use of Temporary Shielding or Locked High Radiation Areas        10
Attachment 2
                and Very High Radiation Area Barricades
Attachment 2
RPP 02-105      RWP                                                              33
AP 22-01        Conduct of Pre-Job and Post-Job Briefs                          9A
Significance Determination Process for Noncited Violation 2009005-16: Operator Actions
AP 25A-200      Access to Locked High or Very High Radiation Areas              20
Disable Circuit Breaker Coordination and Could Initiate Secondary Fires
SEC 01-206      High Security Key Control and Issue                              32
AP 25B-200      Radiography Guidelines                                          12
Introduction
RADIATION WORK PERMITS
93021          9220                92602            93230
This attachment discusses the risk significance of Noncited Violation 2009005-16.  This
Section 4OA2: Identification and Resolution of Problems
document discusses the methods, assumptions, and results of the significance determination
MISCELLANEOUS
process.
      NUMBER                                    TITLE                      REVISION
  SYS AF-200              High Pressure Heater Operations                          8
Methods
  AP 21-001                Conduct of Operations                                  43
  AP 19E-002              Reactivity Management Program                          13
The significance of this finding was evaluated using the significance determination process in
CONDITION REPORTS
Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process,
  CR 18034        CR 04293            CR 2001-2255
because it affected fire protection defense-in-depth strategies involving post-fire safe shutdown
                                        A-23                              Attachment 1
systems. 
This finding was associated with the post-fire safe shutdown category.  Specifically, the
performance deficiency resulted in loss of power to equipment assumed affected in the safe
shutdown analysis and could initiate secondary fires in plant locations outside of the initial fire
area.  The inspectors assigned this finding a high degradation rating since the affected circuit
breakers would not provide any fire protection benefit and would receive no fire protection
credit.
The inspectors assigned a duration factor of 1.00 since the performance deficiency existed for
greater than 30 days.  The inspectors performed a Phase 1 quantitative screening using generic
fire ignition frequencies for the 13 fire areas of concern.  The results of this Phase 1 screening
concluded that a Phase 2 evaluation was needed.
The inspectors followed the guidance in Manual Chapter 0609, Appendix F, Fire Protection
Significance Determination Process, to perform the Phase 2 evaluation. In accordance with
Appendix F, the inspectors used several spreadsheets from NUREG-1805, Fire Dynamics
Tools (FDTs) Quantitative Fire Hazard Analysis Methods for the U.S. Nuclear Regulatory
Commission Fire Protection Inspection Program. The inspectors used the following
spreadsheets in the Phase 2 evaluation:
   
*
02.1_Temperature_NV
*
02.2_Temperature_FV
*
05.1_Heat_Flux_Calculations_Wind_Free
*
9_Plume_Temperature_Calculations
*
10_Detector_Activation_Times
   
The inspectors used these spreadsheets to determine the temperature of the plume, the
temperature of the hot gas layer, and the activation time of the detection systems.


Section 40A5: Other Activities (TI-172 Dissimilar Metal Welds)
MISCELLANEOUS
      NUMBER                                    TITLE                        REVISION
A2-2
  UT-95                  Ultrasonic Examination of Austenitic Piping Welds        3
  WCRE-24                WESDYNE Year 2009 Reactor Vessel Nozzle Safe-            0
                        end Examinations Program Plan
   
  WDI-CAL-102            Calibration Inspection Procedure for PCI Eddy            1
                        Current Card
Attachment 2
                        Installation and Removal of the WESDYNE Nozzle          4
Assumptions
  WDI-EQPT-1021
                        Scanner (SQUID)
The inspectors used the following assumptions during the Phase 2 evaluation:
  WDI-EQPT-1022          Reactor Vessel Nozzle Scanner Setup and Checkout        2
  WDI-STD-146            ET Examination of Reactor Vessel Pipe Welds Inside      9
1. The inspectors assumed that the smoke detectors were located at the maximum possible
                        Surface
distance from the ignition source given the spacing of detectors in each fire area.
                                        A-24                                Attachment 1
2. The inspectors assumed that the detection systems worked properly to detect the fire.
3. The inspectors assumed that the fixed suppression systems would fail to suppress the fire. 
The inspectors assumed the only method of suppressing the fire was manual fire fighting by
the fire brigade.
   
4. The inspectors assumed that operators would take the prescribed mitigating actions during
any fire scenario that progressed to the point where the power-operated relief valve
spuriously opened and its block valve failed to close.  These mitigating actions include steps
for the operators to remove the 125 Vdc control power to the train affected by the fire.
   
5. The licensee concluded that an inter-cable hot short in thermoset cables was needed for a
power-operated relief valve to spuriously open.  Using guidance in Appendix F, Table 2.8.3,
PSP Factors Dependent on Cable Type and Failure Mode, the inspectors assumed the
conditional probability of an inter-cable hot short given a fire scenario that damaged the
thermoset cables was 0.02.
6. The licensee performed an evaluation of the equipment affected by the loss of 125 Vdc
control power. The inspectors reviewed the evaluation and concluded that the loss of
125 Vdc control power did not directly affect the equipment relied upon for post-fire safe
shutdown in each of the fire areas.
7. Without any additional knowledge of the cable routing for the set of affected equipment, the
inspectors assumed that cables for the affected equipment were routed in the same cable
trays as cables for the power-operated relief valves or the associated block valves.
8. The inspectors assumed that any equipment that experienced a loss of dc control power
would experience a short to ground that would lead to a secondary fire in another plant
location.
   
9. The inspectors assumed that a secondary fire in another plant location would damage the
equipment relied upon for safe shutdown in the original fire area and would lead to core
damage. As such, the inspectors provided no credit for the designated post-fire safe
shutdown equipment.
10. The inspectors assumed that the change in core damage frequency associated with the
performance deficiency resulted from the increased likelihood of secondary fires because of  
the loss of circuit breaker protection.


                                            Attachment 2
Significance Determination Process for Noncited Violation 2009005-16: Operator Actions
Disable Circuit Breaker Coordination and Could Initiate Secondary Fires
A2-3
Introduction
This attachment discusses the risk significance of Noncited Violation 2009005-16. This
document discusses the methods, assumptions, and results of the significance determination
process.
Methods
Attachment 2  
The significance of this finding was evaluated using the significance determination process in
Evaluation
Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process,
because it affected fire protection defense-in-depth strategies involving post-fire safe shutdown
During the inspection, the licensee provided information for each of the 13 fire areas, with the
systems.
exception of the reactor building, which is not readily accessible during power operations.  The
This finding was associated with the post-fire safe shutdown category. Specifically, the
information provided included the location of the power-operated relief valve cables (targets); a
performance deficiency resulted in loss of power to equipment assumed affected in the safe
description and photographs of the nearest set of ignition sources near each target; and a
shutdown analysis and could initiate secondary fires in plant locations outside of the initial fire
discussion of the room dimensions, ventilation, and fire protection features.
area. The inspectors assigned this finding a high degradation rating since the affected circuit
breakers would not provide any fire protection benefit and would receive no fire protection
The inspectors performed a field walkdown to verify the information provided by the licensee.  In
credit.
particular, the inspectors verified the spatial arrangement of the fire sources and targets as well
The inspectors assigned a duration factor of 1.00 since the performance deficiency existed for
as the distances between each source and target. The inspectors used the zone of influence
greater than 30 days. The inspectors performed a Phase 1 quantitative screening using generic
described in Appendix F, step 2.3, Fire Scenario Identification and Ignition Source Screening,  
fire ignition frequencies for the 13 fire areas of concern. The results of this Phase 1 screening
to determine the fire sources that could lead to fire scenarios that damaged the power-operated
concluded that a Phase 2 evaluation was needed.
relief valves. These scenarios involved cases where the initial fire directly damaged the cables
The inspectors followed the guidance in Manual Chapter 0609, Appendix F, Fire Protection
as well as situations where the fire propagated through a set of cable trays that contained the  
Significance Determination Process, to perform the Phase 2 evaluation. In accordance with
power-operated relief valve cables.
Appendix F, the inspectors used several spreadsheets from NUREG-1805, Fire Dynamics
Tools (FDTs) Quantitative Fire Hazard Analysis Methods for the U.S. Nuclear Regulatory
The inspectors reviewed the Wolf Creek Generating Station Individual Plant Examination of
Commission Fire Protection Inspection Program. The inspectors used the following
External Events, the fire hazards analysis, and drawings showing the cable routing for the  
spreadsheets in the Phase 2 evaluation:
power-operated relief valves and their associated block valves inside containment. The  
    *  02.1_Temperature_NV
inspectors screened out fire scenarios involving the reactor building given the lack of ignition
    *  02.2_Temperature_FV
sources located under the power-operated relief valve cables.
    *  05.1_Heat_Flux_Calculations_Wind_Free
    *  9_Plume_Temperature_Calculations
The inspectors used the Fire Dynamics Tools to calculate the temperature of the hot gas layer
    *  10_Detector_Activation_Times
in each fire area. The inspectors concluded that the hot gas layer would never reach a high
The inspectors used these spreadsheets to determine the temperature of the plume, the
enough temperature to damage the thermoset cables.  Therefore, the inspectors screened out
temperature of the hot gas layer, and the activation time of the detection systems.
all fire scenarios involving a hot gas layer that would damage the power-operated relief valve.  
                                              A2-1                                  Attachment 2
Based on the walkdown and hot gas layer evaluations, the inspectors created an initial set of  
five fire sources involving nine fire scenarios that could lead to core damage. The scenarios are
listed in the following table.  The categories assigned to components and values determined
related to the Source Category, Fire Ignition Frequency, Heat Release Rate, and Severity
Factor used to characterize the fire scenarios in the significance determination process are
described in Manual Chapter 0609, Appendix F.  The inspectors summarized the fire scenarios
in Table 1, Initial Fire Scenarios.
Fire Scenarios
The detailed evaluation of each ignition source is provided below. In each of these scenarios,
the inspectors used the Fire Dynamics Tools to calculate the time to damage the
power-operated relief valve and block valve cables and the time to detect the fire. As noted
above, the inspectors assumed that the fixed suppression systems failed to suppress the fire
and the only method of suppression resulted from manual fire fighting from the fire brigade.  
The inspectors used Manual Chapter 0609, Appendix F, Attachment 8, Table A8.1,
Non-Suppression Probability Values for Manual Fire Fighting Based on Fire Duration Time to
Damage after Detection) and Fire Type Category to calculate the non-suppression probability
for manual fire fighting.  The results are different for each scenarios based on the type of fire
and the length of time between the detection of the fire and damage to the cables.  


Assumptions
The inspectors used the following assumptions during the Phase 2 evaluation:
1. The inspectors assumed that the smoke detectors were located at the maximum possible
A2-4
    distance from the ignition source given the spacing of detectors in each fire area.
2. The inspectors assumed that the detection systems worked properly to detect the fire.
3. The inspectors assumed that the fixed suppression systems would fail to suppress the fire.
    The inspectors assumed the only method of suppressing the fire was manual fire fighting by
    the fire brigade.
Attachment 2
4. The inspectors assumed that operators would take the prescribed mitigating actions during
Table 2. Initial Fire Scenarios
    any fire scenario that progressed to the point where the power-operated relief valve
Scenario
    spuriously opened and its block valve failed to close. These mitigating actions include steps
Number
    for the operators to remove the 125 Vdc control power to the train affected by the fire.
Ignition
5. The licensee concluded that an inter-cable hot short in thermoset cables was needed for a
Source
    power-operated relief valve to spuriously open. Using guidance in Appendix F, Table 2.8.3,
Source
    PSP Factors Dependent on Cable Type and Failure Mode, the inspectors assumed the
Description
    conditional probability of an inter-cable hot short given a fire scenario that damaged the
(Fire Area)
    thermoset cables was 0.02.
Source
6. The licensee performed an evaluation of the equipment affected by the loss of 125 Vdc
Category
    control power. The inspectors reviewed the evaluation and concluded that the loss of
Initial Fire
    125 Vdc control power did not directly affect the equipment relied upon for post-fire safe
Ignition
    shutdown in each of the fire areas.
Frequency
7. Without any additional knowledge of the cable routing for the set of affected equipment, the
Heat
    inspectors assumed that cables for the affected equipment were routed in the same cable
Release
    trays as cables for the power-operated relief valves or the associated block valves.
Rate
8. The inspectors assumed that any equipment that experienced a loss of dc control power
Severity
    would experience a short to ground that would lead to a secondary fire in another plant
Factor
    location.
Fire
9. The inspectors assumed that a secondary fire in another plant location would damage the
Targets
    equipment relied upon for safe shutdown in the original fire area and would lead to core
Nearest
    damage. As such, the inspectors provided no credit for the designated post-fire safe
Distance
    shutdown equipment.
1  
10. The inspectors assumed that the change in core damage frequency associated with the
RP-333
    performance deficiency resulted from the increased likelihood of secondary fires because of
Relay
    the loss of circuit breaker protection.
Panel
                                            A2-2                                    Attachment 2
(A-16)
General
Control
Cabinet
6.00E-5
200 kW
0.9
4U3B
4U3A
4.8 ft
2  
RP-333
Relay
Panel
(A-16)
General
Control
Cabinet
6.00E-5
650 kW
0.1
4U3B
4U3A
4.8 ft
3  
SK194B
Security
Panel
(A-16)
General
Electrical
Cabinet
6.00E-5
200 kW
0.1
4U3B
4U3A
5.0 ft
4  
NG01B
600 V
MCC
(A-18)
General
Electrical
Cabinet
6.00E-5
70 kW
0.9
1U3J
1U3K
3.3 ft
5  
NG01B
600 V
MCC
(A-18)
General
Electrical
Cabinet
6.00E-5
200 kW
0.1
1U3J
1U3K
3.3 ft
6
Transients
C-21
Transients
(Medium)
1.70E-4
70 kW
0.9
1C8H
1C8J
1.3 ft
7
Transients
C-21
Transients
(Medium)
1.70E-4
200 kW
0.1
1C8H
1C8J
1.3 ft
8
Transients
C-22
Transients
(Medium)
1.70E-4
70 kW
0.9
4C8E
4C8F
0.0 ft
9
Transients
C-22
Transients
(Medium)
1.70E-4
200 kW
0.1
4C8E
4C8F
0.0 ft
1. Source RP-333
Panel RP-333 is a relay panel located against a wall in Fire Area A-16. The top of the cabinet is
7 10 from the floor. The inspectors treated the relay panel as a general control cabinet with a  
fire ignition frequency of 6.00E-5 and heat release rates of 200 kW and 650 kW.  
The power-operated relief valve cables are located in cable tray 4U3B and the power-operated
relief valve block valve cables are located in cable tray 4U3A.  Cable tray 4U3B is the third tray
and cable tray 4U3A is the fourth tray from the bottom of a stack of cable trays.  The lowest
cable tray is located 11 8 from the floor.
Fire Area A-16 is protected by a single zone smoke detection system with a maximum distance
of 25 feet between detectors.  Areas of cable tray concentration contain preaction sprinkler
systems for fixed fire suppression.  


Evaluation
During the inspection, the licensee provided information for each of the 13 fire areas, with the
exception of the reactor building, which is not readily accessible during power operations. The
A2-5
information provided included the location of the power-operated relief valve cables (targets); a
description and photographs of the nearest set of ignition sources near each target; and a
discussion of the room dimensions, ventilation, and fire protection features.
The inspectors performed a field walkdown to verify the information provided by the licensee. In
particular, the inspectors verified the spatial arrangement of the fire sources and targets as well
Attachment 2
as the distances between each source and target. The inspectors used the zone of influence
Scenario 1 - Heat Release Rate (200 kW)
described in Appendix F, step 2.3, Fire Scenario Identification and Ignition Source Screening,
to determine the fire sources that could lead to fire scenarios that damaged the power-operated
The inspectors calculated a plume temperature of 1178°F, corresponding to a damage time of 1
relief valves. These scenarios involved cases where the initial fire directly damaged the cables
minute for the lowest cable tray and a damage time of 10 minutes for the target set.  The
as well as situations where the fire propagated through a set of cable trays that contained the
inspectors calculated a detection time less than 1 minute.  The inspectors assigned a
power-operated relief valve cables.
non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes
The inspectors reviewed the Wolf Creek Generating Station Individual Plant Examination of
between the time to detection and time to damage.  
External Events, the fire hazards analysis, and drawings showing the cable routing for the
power-operated relief valves and their associated block valves inside containment. The
Scenario 2 - Heat Release Rate (650 kW)  
inspectors screened out fire scenarios involving the reactor building given the lack of ignition
sources located under the power-operated relief valve cables.
The inspectors calculated a plume temperature exceeding 2000°F, corresponding to a damage
The inspectors used the Fire Dynamics Tools to calculate the temperature of the hot gas layer
time of 1 minute for the lowest cable tray and a damage time of 10 minutes for the target set.
in each fire area. The inspectors concluded that the hot gas layer would never reach a high
The inspectors calculated a detection time less than 1 minute. The inspectors assigned a
enough temperature to damage the thermoset cables. Therefore, the inspectors screened out
non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes
all fire scenarios involving a hot gas layer that would damage the power-operated relief valve.
between the time to detection and time to damage.  
Based on the walkdown and hot gas layer evaluations, the inspectors created an initial set of
five fire sources involving nine fire scenarios that could lead to core damage. The scenarios are
2. Source SK194B
listed in the following table. The categories assigned to components and values determined
related to the Source Category, Fire Ignition Frequency, Heat Release Rate, and Severity
Panel SK194B is a security panel located against a wall in Fire Area A-16. The top of the  
Factor used to characterize the fire scenarios in the significance determination process are
cabinet is 7 8 from the floor. The inspectors treated the security panel as a general electrical
described in Manual Chapter 0609, Appendix F. The inspectors summarized the fire scenarios
cabinet with a fire ignition frequency of 6.00E-5 and heat release rates of 70 kW and 200 kW.
in Table 1, Initial Fire Scenarios.
Using a zone of influence, the inspectors screened out the lower heat release rate during the  
Fire Scenarios
plant walkdown.
The detailed evaluation of each ignition source is provided below. In each of these scenarios,
the inspectors used the Fire Dynamics Tools to calculate the time to damage the
The power-operated relief valve cables are located in cable tray 4U3B and the power-operated  
power-operated relief valve and block valve cables and the time to detect the fire. As noted
relief valve block valve cables are located in cable tray 4U3A. Cable tray 4U3B is the third tray
above, the inspectors assumed that the fixed suppression systems failed to suppress the fire
and cable tray 4U3A is the fourth tray from the bottom of a stack of cable trays. The lowest
and the only method of suppression resulted from manual fire fighting from the fire brigade.
cable tray is located 11 8 from the floor.  
The inspectors used Manual Chapter 0609, Appendix F, Attachment 8, Table A8.1,
Non-Suppression Probability Values for Manual Fire Fighting Based on Fire Duration Time to
Fire Area A-16 is protected by a single zone smoke detection system with a maximum distance
Damage after Detection) and Fire Type Category to calculate the non-suppression probability
of 25 feet between detectors. Areas of cable tray concentration contain preaction sprinkler
for manual fire fighting. The results are different for each scenarios based on the type of fire
systems for fixed fire suppression.  
and the length of time between the detection of the fire and damage to the cables.
                                            A2-3                                    Attachment 2
Scenario 3 - Heat Release Rate (200 kW)
The inspectors calculated a plume temperature of 1103°F, corresponding to a damage time of 1
minute for the lowest cable tray and a damage time of 10 minutes for the target set. The
inspectors calculated a detection time less than 1 minute. The inspectors assigned a
non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes
between the time to detection and time to damage.
3. Source NG01B
Panel NG01B is a 600V motor control center located in the open in Fire Area A-18.  The top of  
the cabinet is 7 8 from the floor.  The inspectors treated the motor control center as a general
electrical cabinet with a fire ignition frequency of 6.00E-5 and heat release rates of 70 kW and
200 kW.  


                                    Table 2. Initial Fire Scenarios
                          Source                Initial Fire  Heat
   
  Scenario      Ignition              Source                          Severity    Fire    Nearest
A2-6  
                        Description              Ignition    Release
  Number      Source                Category                          Factor  Targets    Distance
                        (Fire Area)            Frequency      Rate
                        Relay      General
                                                                                4U3B
Attachment 2  
    1      RP-333    Panel      Control      6.00E-5    200 kW    0.9                  4.8 ft
The power-operated relief valve cables are located in cable tray 1U3J and the power-operated
                                                                                4U3A
relief valve block valve cables are located in cable tray 1U3K. Cable tray 1U3J is the third tray
                        (A-16)      Cabinet
and cable tray 1U3K is the second tray from the bottom of a stack of cable trays. The lowest
                        Relay      General
cable tray is located 9 11 from the floor.  
                                                                                4U3B
    2       RP-333    Panel      Control      6.00E-5    650 kW    0.1                  4.8 ft
Fire Area A-18 is protected by a cross zone smoke detection system with a maximum distance
                                                                                4U3A
of 5 feet between detectors. A total flooding halon system provides fixed fire suppression.  
                        (A-16)      Cabinet
                        Security    General
Scenario 4 - Heat Release Rate (70 kW)  
                                                                                4U3B
    3      SK194B    Panel      Electrical    6.00E-5     200 kW    0.1                  5.0 ft
The inspectors calculated a plume temperature of 421°F. Since this is less than the damage
                                                                                4U3A
threshold of 625 °F for thermoset cables, the inspectors screened out this scenario from further
                        (A-16)     Cabinet
consideration.
                        600 V      General
                                                                                1U3J
Scenario 5 - Heat Release Rate (200 kW)  
    4      NG01B      MCC        Electrical    6.00E-5      70 kW    0.9                  3.3 ft
                                                                                1U3K
The inspectors calculated a plume temperature of 1019°F, corresponding to a damage time of 1  
                        (A-18)      Cabinet
minute for the lowest cable tray and a damage time of 8 minutes for the target set. The
                        600 V      General
inspectors calculated a detection time less than 1 minute. The inspectors assigned a
                                                                                1U3J
non-suppression probability for manual fire fighting of 0.44 for an electrical fire with 7 minutes
    5       NG01B      MCC        Electrical    6.00E-5    200 kW   0.1                  3.3 ft
between the time to detection and time to damage.  
                                                                                1U3K
                        (A-18)     Cabinet
4. Transient Combustibles in Fire Area C-21 (Lower Cable Spreading Room)  
                                    Transients                                  1C8H
Fire Area C-21 has a length of 88 and a width of 66. The area is protected by a single zone
    6      Transients C-21                      1.70E-4      70 kW    0.9                  1.3 ft
smoke detection system with a maximum distance of 15 feet between detectors.  A preaction
                                    (Medium)                                    1C8J
sprinkler system provides fixed fire suppression.  
                                    Transients                                  1C8H
The power-operated relief valve cables are located in cable tray 1C8H and the power-operated  
    7      Transients C-21                      1.70E-4    200 kW    0.1                  1.3 ft
relief valve block valve cables are located in cable tray 1C8J. Cable tray 1C8H is the fifth tray  
                                    (Medium)                                    1C8J
and cable tray 1U3K is the fourth tray from the bottom of a stack of cable trays. The lowest  
                                    Transients                                  4C8E
cable tray is located 3 4 from the floor.  
    8      Transients C-22                      1.70E-4     70 kW    0.9                  0.0 ft
                                    (Medium)                                    4C8F
The inspectors determined that the cables for both valves were located in the same cable tray
                                    Transients                                  4C8E
stack for approximately 107 feet and the same cable tray for approximately 8 feet.  For the
    9      Transients C-22                      1.70E-4    200 kW    0.1                  0.0 ft
Phase 2 evaluation, the inspectors conservatively assumed that the cables for both valves were
                                    (Medium)                                     4C8F
located in the lower tray through the entire area.  The inspectors assumed that the cables trays
1. Source RP-333
were 2 feet wide.
Panel RP-333 is a relay panel located against a wall in Fire Area A-16. The top of the cabinet is
7 10 from the floor. The inspectors treated the relay panel as a general control cabinet with a
For the following two scenarios, the inspectors adjusted the fire ignition frequency to account for
fire ignition frequency of 6.00E-5 and heat release rates of 200 kW and 650 kW.
the limited areas where a fire could damage the targets.  The inspectors modified the transient
The power-operated relief valve cables are located in cable tray 4U3B and the power-operated
combustible fire ignition frequency by multiplying the initial fire ignition frequency by a weighting
relief valve block valve cables are located in cable tray 4U3A. Cable tray 4U3B is the third tray
factor.  The inspectors calculated the weighting factor by dividing the surface area of the cables
and cable tray 4U3A is the fourth tray from the bottom of a stack of cable trays. The lowest
trays containing cables for both valves by the area of the fire area.  The inspectors calculated a  
cable tray is located 11 8 from the floor.
modified fire ignition frequency for transient combustibles of 6.26E-6.  
Fire Area A-16 is protected by a single zone smoke detection system with a maximum distance
of 25 feet between detectors. Areas of cable tray concentration contain preaction sprinkler
Scenario 6 - Heat Release Rate (70 kW)
systems for fixed fire suppression.
                                              A2-4                                  Attachment 2
The inspectors calculated a plume temperature of 943°F, corresponding to a damage time of 1
minute for the lowest cable tray and a damage time of 11 minutes for the target set. The
inspectors calculated a detection time less than 1 minute.  The inspectors assigned a


Scenario 1 - Heat Release Rate (200 kW)
The inspectors calculated a plume temperature of 1178°F, corresponding to a damage time of 1
minute for the lowest cable tray and a damage time of 10 minutes for the target set. The
A2-7
inspectors calculated a detection time less than 1 minute. The inspectors assigned a
non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes
between the time to detection and time to damage.
Scenario 2 - Heat Release Rate (650 kW)
The inspectors calculated a plume temperature exceeding 2000°F, corresponding to a damage
Attachment 2
time of 1 minute for the lowest cable tray and a damage time of 10 minutes for the target set.
non-suppression probability for manual fire fighting of 0.26 for transient fires with 10 minutes  
The inspectors calculated a detection time less than 1 minute. The inspectors assigned a
between the time to detection and time to damage.  
non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes
between the time to detection and time to damage.
Scenario 7 - Heat Release Rate (200 kW)  
2. Source SK194B
Panel SK194B is a security panel located against a wall in Fire Area A-16. The top of the
The inspectors calculated a plume temperature exceeding 2000°F, corresponding to a damage  
cabinet is 7 8 from the floor. The inspectors treated the security panel as a general electrical
time of 1 minute for the lowest cable tray and a damage time of 11 minutes for the target set.
cabinet with a fire ignition frequency of 6.00E-5 and heat release rates of 70 kW and 200 kW.
The inspectors calculated a detection time less than 1 minute. The inspectors assigned a  
Using a zone of influence, the inspectors screened out the lower heat release rate during the
non-suppression probability for manual fire fighting of 0.26 for transient fires with 10 minutes  
plant walkdown.
between the time to detection and time to damage.  
The power-operated relief valve cables are located in cable tray 4U3B and the power-operated
relief valve block valve cables are located in cable tray 4U3A. Cable tray 4U3B is the third tray
5. Transient Combustibles in Fire Area C-22 (Upper Cable Spreading Room)
and cable tray 4U3A is the fourth tray from the bottom of a stack of cable trays. The lowest
cable tray is located 11 8 from the floor.
Fire Area C-22 has a length of 88 and a width of 67. The power-operated relief valve cables  
Fire Area A-16 is protected by a single zone smoke detection system with a maximum distance
are located in cable trays 4C8E, 4C8F, and 4C8G and the power-operated relief valve block  
of 25 feet between detectors. Areas of cable tray concentration contain preaction sprinkler
valve cables are located in cable trays 4C8F and 4C8G.  These cable trays transition into the
systems for fixed fire suppression.
control room through the floor of the upper cable spreading room.
Scenario 3 - Heat Release Rate (200 kW)
The inspectors calculated a plume temperature of 1103°F, corresponding to a damage time of 1
The inspectors determined that cables for both valves were located in the same cable tray stack
minute for the lowest cable tray and a damage time of 10 minutes for the target set. The
for approximately 96 feet. For the Phase 2 evaluation, the inspectors conservatively assumed
inspectors calculated a detection time less than 1 minute. The inspectors assigned a
that the cables for both valves were located in the same cable tray through the entire area and
non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes
that the cable tray was located on the floor.  The inspectors assumed that the cables trays were
between the time to detection and time to damage.
2 feet wide.  
3. Source NG01B
Panel NG01B is a 600V motor control center located in the open in Fire Area A-18. The top of
The inspectors did not credit the detection or suppression systems for the following two
the cabinet is 7 8 from the floor. The inspectors treated the motor control center as a general
scenarios since the fire was assumed to damage the target set immediately. 
electrical cabinet with a fire ignition frequency of 6.00E-5 and heat release rates of 70 kW and
200 kW.
For the following two scenarios, the inspectors adjusted the fire ignition frequency to account for
                                              A2-5                                    Attachment 2
the limited areas where a fire could damage the targets. The inspectors modified the transient
combustible fire ignition frequency by multiplying the initial fire ignition frequency by a weighting
factor. The inspectors calculated the weighting factor by dividing the surface area of the cables
trays containing cables for both valves by the area of the fire area.  The inspectors calculated a
modified fire ignition frequency for transient combustibles of 5.54E-6.  
Scenario 8 - Heat Release Rate (70 kW)  
The inspectors postulated that the transient fire was located on the cable tray containing the
cables for both valves, corresponding to immediate damage for the target set. The inspectors
assigned a non-suppression probability for manual fire fighting of 1.00 for transient fires with no
time between detection and damage.  
Scenario 9 - Heat Release Rate (200 kW)
The inspectors postulated that the transient fire was located on the cable tray containing the  
cables for both valves, corresponding to immediate damage for the target set. The inspectors  
assigned a non-suppression probability for manual fire fighting of 1.00 for transient fires with no
time between detection and damage.  


The power-operated relief valve cables are located in cable tray 1U3J and the power-operated
relief valve block valve cables are located in cable tray 1U3K. Cable tray 1U3J is the third tray
and cable tray 1U3K is the second tray from the bottom of a stack of cable trays. The lowest
A2-8
cable tray is located 9 11 from the floor.
Fire Area A-18 is protected by a cross zone smoke detection system with a maximum distance
of 5 feet between detectors. A total flooding halon system provides fixed fire suppression.
Scenario 4 - Heat Release Rate (70 kW)
The inspectors calculated a plume temperature of 421°F. Since this is less than the damage
Attachment 2
threshold of 625 °F for thermoset cables, the inspectors screened out this scenario from further
Results
consideration.
Scenario 5 - Heat Release Rate (200 kW)
The inspectors used the Phase 2 evaluation to perform a bounding analysis and determine an
The inspectors calculated a plume temperature of 1019°F, corresponding to a damage time of 1
upper limit for the change in core damage frequency.  In each of the scenarios described above,
minute for the lowest cable tray and a damage time of 8 minutes for the target set. The
the change in core damage frequency was bounded by the conditional core damage probability
inspectors calculated a detection time less than 1 minute. The inspectors assigned a
(CCDP). The inspectors calculated the conditional core damage probability using the following
non-suppression probability for manual fire fighting of 0.44 for an electrical fire with 7 minutes
equation:
between the time to detection and time to damage.
4. Transient Combustibles in Fire Area C-21 (Lower Cable Spreading Room)
Short
Fire Area C-21 has a length of 88 and a width of 66. The area is protected by a single zone
Hot
smoke detection system with a maximum distance of 15 feet between detectors. A preaction
n
sprinkler system provides fixed fire suppression.
Suppressio
The power-operated relief valve cables are located in cable tray 1C8H and the power-operated
Non
relief valve block valve cables are located in cable tray 1C8J. Cable tray 1C8H is the fifth tray
P
and cable tray 1U3K is the fourth tray from the bottom of a stack of cable trays. The lowest
x
cable tray is located 3 4 from the floor.
P
The inspectors determined that the cables for both valves were located in the same cable tray
x
stack for approximately 107 feet and the same cable tray for approximately 8 feet. For the
SF
Phase 2 evaluation, the inspectors conservatively assumed that the cables for both valves were
x
located in the lower tray through the entire area. The inspectors assumed that the cables trays
FIF
were 2 feet wide.
CCDP
For the following two scenarios, the inspectors adjusted the fire ignition frequency to account for
the limited areas where a fire could damage the targets. The inspectors modified the transient
combustible fire ignition frequency by multiplying the initial fire ignition frequency by a weighting
factor. The inspectors calculated the weighting factor by dividing the surface area of the cables
trays containing cables for both valves by the area of the fire area. The inspectors calculated a
modified fire ignition frequency for transient combustibles of 6.26E-6.
Scenario 6 - Heat Release Rate (70 kW)
The inspectors calculated a plume temperature of 943°F, corresponding to a damage time of 1
minute for the lowest cable tray and a damage time of 11 minutes for the target set. The
inspectors calculated a detection time less than 1 minute. The inspectors assigned a
                                            A2-6                                      Attachment 2


non-suppression probability for manual fire fighting of 0.26 for transient fires with 10 minutes
=
between the time to detection and time to damage.
Scenario 7 - Heat Release Rate (200 kW)
The inspectors calculated a plume temperature exceeding 2000°F, corresponding to a damage
where: 
time of 1 minute for the lowest cable tray and a damage time of 11 minutes for the target set.
FIF  denotes the fire ignition frequency  
The inspectors calculated a detection time less than 1 minute. The inspectors assigned a
non-suppression probability for manual fire fighting of 0.26 for transient fires with 10 minutes
between the time to detection and time to damage.
SF  denotes the severity factor  
5. Transient Combustibles in Fire Area C-22 (Upper Cable Spreading Room)
Fire Area C-22 has a length of 88 and a width of 67. The power-operated relief valve cables
are located in cable trays 4C8E, 4C8F, and 4C8G and the power-operated relief valve block
n
valve cables are located in cable trays 4C8F and 4C8G. These cable trays transition into the
Suppressio
control room through the floor of the upper cable spreading room.
Non
The inspectors determined that cables for both valves were located in the same cable tray stack
P
for approximately 96 feet. For the Phase 2 evaluation, the inspectors conservatively assumed
that the cables for both valves were located in the same cable tray through the entire area and
that the cable tray was located on the floor. The inspectors assumed that the cables trays were
2 feet wide.
The inspectors did not credit the detection or suppression systems for the following two
scenarios since the fire was assumed to damage the target set immediately.
For the following two scenarios, the inspectors adjusted the fire ignition frequency to account for
the limited areas where a fire could damage the targets. The inspectors modified the transient
combustible fire ignition frequency by multiplying the initial fire ignition frequency by a weighting
factor. The inspectors calculated the weighting factor by dividing the surface area of the cables
trays containing cables for both valves by the area of the fire area. The inspectors calculated a
modified fire ignition frequency for transient combustibles of 5.54E-6.
Scenario 8 - Heat Release Rate (70 kW)
The inspectors postulated that the transient fire was located on the cable tray containing the
cables for both valves, corresponding to immediate damage for the target set. The inspectors
assigned a non-suppression probability for manual fire fighting of 1.00 for transient fires with no
time between detection and damage.
Scenario 9 - Heat Release Rate (200 kW)
The inspectors postulated that the transient fire was located on the cable tray containing the
cables for both valves, corresponding to immediate damage for the target set. The inspectors
assigned a non-suppression probability for manual fire fighting of 1.00 for transient fires with no
time between detection and damage.
                                            A2-7                                      Attachment 2


Results
denotes the non-suppression probability  
The inspectors used the Phase 2 evaluation to perform a bounding analysis and determine an
upper limit for the change in core damage frequency. In each of the scenarios described above,
the change in core damage frequency was bounded by the conditional core damage probability
Short
(CCDP). The inspectors calculated the conditional core damage probability using the following
Hot
equation:
P
                CCDP = FIF x SF x PNon  Suppression x PHot Short
  denotes the probability of a hot short  
where:          FIF denotes the fire ignition frequency
                SF denotes the severity factor
The sum of the conditional core damage probabilities for each of the fire scenarios bounded the  
                PNon Suppression denotes the non-suppression probability
total change in core damage frequency associated with this performance deficiency. The  
                PHot Short denotes the probability of a hot short
inspectors calculated a bounding value of 6.58E-7 for the change in core damage frequency for  
The sum of the conditional core damage probabilities for each of the fire scenarios bounded the
this performance deficiency. The results from the nine scenarios described above are  
total change in core damage frequency associated with this performance deficiency. The
contained in the following table:  
inspectors calculated a bounding value of 6.58E-7 for the change in core damage frequency for
this performance deficiency. The results from the nine scenarios described above are
contained in the following table:
                                                A2-8                            Attachment 2


                          Table 3. Phase 2 Evaluation Results
Scenario   Ignition   Fire Ignition   Severity     Probability of Probability of
                                                                                        CCDP
A2-9
Number      Source      Frequency        Factor    Non-Suppression   a Hot Short
  1       RP-333       6.00E-5         0.9           0.35           0.02           3.78E-7
  2       RP-333       6.00E-5         0.1           0.35           0.02           4.20E-8
  3       SK194B       6.00E-5         0.1           0.35           0.02           4.20E-8
  4       NG01B         6.00E-5         0.9           N/A           N/A             N/A
Attachment 2
  5       NG01B         6.00E-5         0.1           0.44           0.02           5.28E-8
        Transient Fire
Table 3. Phase 2 Evaluation Results  
  6                      6.26E-6         0.9           0.26           0.02           2.93E-8
Scenario  
            (C-21)
Number
        Transient Fire
Ignition  
  7                      6.26E-6         0.1           0.26           0.02           3.26E-9
Source
            (C-21)
Fire Ignition  
        Transient Fire
Frequency
  8                      5.54E-6         0.9           1.00           0.02           9.96E-8
Severity  
            (C-22)
Factor
        Transient Fire
Probability of  
  9                      5.54E-6         0.1           1.00           0.02           1.11E-8
Non-Suppression  
            (C-22)
Probability of
                                                                        Total         6.58E-7
a Hot Short  
                                      A2-9                                      Attachment 2
CCDP
1  
RP-333  
6.00E-5  
0.9  
0.35  
0.02  
3.78E-7  
2  
RP-333  
6.00E-5  
0.1  
0.35  
0.02  
4.20E-8  
3  
SK194B  
6.00E-5  
0.1  
0.35  
0.02  
4.20E-8  
4  
NG01B  
6.00E-5  
0.9  
N/A  
N/A  
N/A  
5  
NG01B  
6.00E-5  
0.1  
0.44  
0.02  
5.28E-8  
6
Transient Fire  
(C-21)
6.26E-6  
0.9  
0.26  
0.02  
2.93E-8  
7
Transient Fire
(C-21)  
6.26E-6  
0.1  
0.26  
0.02  
3.26E-9  
8
Transient Fire
(C-22)  
5.54E-6  
0.9  
1.00  
0.02  
9.96E-8  
9
Transient Fire
(C-22)  
5.54E-6  
0.1  
1.00  
0.02  
1.11E-8  
Total  
6.58E-7
}}
}}

Latest revision as of 06:37, 14 January 2025

IR 05000482-09-005, on 10/01/2009 - 12/31/2009; Wolf Creek Generating Station, Integrated Resident and Regional Report; Fire Protection, Inservice Inspection Activities; Maintenance Risk Assessments and Emergent Work Controls
ML100430713
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 02/11/2010
From: Geoffrey Miller
NRC/RGN-IV/DRP/RPB-B
To:
References
ea-10-004, EA-10-020
Download: ML100430713 (118)


See also: IR 05000482/2009005

Text

February 11, 2010

EA-10-004

EA-10-020

Matthew W. Sunseri, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

SUBJECT:

WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION

REPORT 05000482/2009005 AND NOTICE OF VIOLATIONS

Dear Mr. Sunseri:

On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Wolf Creek Generating Station. The enclosed integrated inspection report

documents the inspection findings, which were discussed on January 14, 2010, with you and

other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the NRC has identified two issues that were evaluated

under the risk significance determination process as having very low safety significance (green).

The NRC has also determined that violations are associated with these issues. One violation

involved failure to implement corrective actions to address refueling water storage tank leakage

(EA-10-004). The second violation involved failure to correct an inadequate reactor vessel head

vent path (EA-10-020). These violations were evaluated in accordance with the NRC

Enforcement Policy included on the NRCs Web site at www.nrc.gov/about-

nrc/regulatory/enforcement/enforce-pol.html.

The violations are being cited in the enclosed Notice of Violations (Notice) and the

circumstances surrounding them are described in detail in the subject inspection report. The

violations are being cited in the Notice because Wolf Creek Generating Station failed to restore

compliance within a reasonable time after the violations were identified in NRC Inspection

Reports05000482/2007003-006 and 05000482/2008004-007, as specified in Section VI.A.1 of

the NRC Enforcement Policy.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. The NRC will use your response, in part, to

UNITED STATES

NUCLEAR REGULATORY COMMISSION

R E GI ON I V

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

Wolf Creek Nuclear Operating Corporation - 2 -

- 2 -

determine whether further enforcement action is necessary to ensure compliance with

regulatory requirements.

Based on the results of this inspection, the NRC has also determined that one additional

Severity Level IV violation of NRC requirements occurred. This report also documents

12 NRC identified and one self-revealing finding of very low safety significance (Green). All of

these findings were determined to involve violations of NRC requirements. Additionally, two

licensee-identified violations, which were determined to be of very low safety significance, are

listed in this report. However, because of the very low safety significance and because they are

entered into your corrective action program, the NRC is treating these findings as noncited

violations, consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest the

violations or the significance of the noncited violations, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with

copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 612 E.

Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident

Inspector at the Wolf Creek Generating Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its

enclosure, will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

Geoffrey B. Miller, Chief

Project Branch B

Division of Reactor Projects

Docket No. 50-482

License No. NPF-42

Enclosure

Inspection Report 05000482/2009005

w/Attachment: Supplemental Information

Wolf Creek Nuclear Operating Corporation - 3 -

- 3 -

cc w/Enclosure:

Vice President Operations/Plant Manager

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Jay Silberg, Esq.

Pillsbury Winthrop Shaw Pittman LLP

2300 N Street, NW

Washington, DC 20037

Supervisor Licensing

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, KS 66839

Chief Engineer

Utilities Division

Kansas Corporation Commission

1500 SW Arrowhead Road

Topeka, KS 66604-4027

Office of the Governor

State of Kansas

Topeka, KS 66612

Attorney General

120 S.W. 10th Avenue, 2nd Floor

Topeka, KS 66612-1597

County Clerk

Coffey County Courthouse

110 South 6th Street

Burlington, KS 66839

Chief, Radiation and Asbestos

Control Section

Kansas Department of Health and

Environment

Bureau of Air and Radiation

1000 SW Jackson, Suite 310

Topeka, KS 66612-1366

Wolf Creek Nuclear Operating Corporation - 4 -

- 4 -

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRP Deputy Director (Anton.Vegel@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (Chris.Long@nrc.gov)

Site Secretary (Shirley.Allen@nrc.gov)

Branch Chief, DRP/B (Geoffrey.Miller@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

Senior Public Affairs Officer (Victor.Dricks@nrc.gov)

Senior Public Affairs Officer (Lara.Uselding@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Only inspection reports to the following:

DRS/TSB STA (Dale.Powers@nrc.gov)

L. Trocine, OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)

ROPreports

File located: R:\\_REACTORS\\_WC\\2009\\WC20090005-RP-CML.doc ML 100430713

SUNSI Rev Compl.

Yes No

ADAMS

Yes No

Reviewer Initials

GBM

Publicly Avail

Yes No

Sensitive

Yes : No

Sens. Type Initials

GBM

RI:DRP/

SRI:DRP/

SPE:DRP/

C:DRS/EB1

C:DRS/EB2

CAPeabody

CMLong

RDeese

TFarnholtz

NFOKeefe

/RA/GMiller for

/RA/GMiller for

/RA/

/RA/

/RA/

01/22/2010

01/29/2010

02/05/2010

02/05/2010

02/05/2010

C:DRS/OB

C:DRS/PSB1

C:DRS/PSB2

RIV:ACES

C:DRP/

SGarchow

MPShannon

GEWerner

RKellar

GBMiller

/RA/

/RA/

/RA/

/RA/

/RA/

02/09/2010

02/08/2010

02/09/2010

02/09/2010

02/11010

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

- 1 -

Enclosure 1

NOTICE OF VIOLATIONS

Wolf Creek Nuclear Operating Corporation

Docket: 50-482

Wolf Creek Generating Station

License: NPF-42

EA-10-004

EA-10-020

During an NRC inspection conducted October 1 through December 31, 2009, two violations of

NRC requirements were identified. In accordance with the NRC Enforcement Policy, the

violations are listed below:

A.

Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires,

in part, that measures shall be established to assure that conditions adverse

to quality are promptly identified and corrected.

Contrary to the above, from 1998 to December 31, 2009, the measures

established by Wolf Creek did not correct a condition adverse to quality.

Specifically, Wolf Creek did not correct leakage from the refueling water

storage tank.

This violation is associated with a Green Significance Determination Process finding

(EA-10-004).

B.

Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that

the design basis is correctly translated into specifications, drawings, and procedures.

The design basis of the reactor vessel head vent is to allow noncondensable gases to

escape to the pressurizer during shutdown conditions.

Contrary to the above, from December 2, 2003, to December 31, 2009, Wolf Creek

failed to ensure the design basis of the reactor vessel head vent was correctly translated

into specifications, drawings and procedures. Specifically, Wolf Creek designed and

installed a reactor vessel head permanent vent piping modification which failed to vent

noncondensable gases to the pressurizer during shutdown operations.

This resulted in the formation of voids in the reactor vessel head while the plant was

shutdown and depressurized in successive refueling outages.

This violation is associated with a Green Significance Determination Process finding

(EA-10-020).

Pursuant to the provisions of 10 CFR 2.201, Wolf Creek Nuclear Operating Corporation is

hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555, with a copy to the

Regional Administrator, Region IV, and a copy to the NRC Senior Resident Inspector at the

facility that is the subject of this Notice of Violation (Notice), within 30 days of the date of the

letter transmitting this Notice. This reply should be clearly marked as a "Reply to Notice of

Violation EA-10-004," EA 10-020, and should include for each violation (1) the reason for the

- 2 -

Enclosure 1

violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective

steps that have been taken and the results achieved, (3) the corrective steps

That will be taken to avoid further violations, and (4) the date when full compliance will be

achieved. Your response may reference or include previous docketed correspondence, if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an Order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not

include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the bases for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information. If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 11h day of February 2010

- 1 -

Enclosure 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

05000482

License:

NPF-42

Report:

05000482/2009005

Licensee:

Wolf Creek Operating Corporation

Facility:

Wolf Creek Generating Station

Location:

1550 Oxen Lane SE

Burlington, Kansas

Dates:

October 1 through December 31, 2009

Inspectors:

C. M. Long, Senior Resident Inspector

R. A. Kopriva, Senior Reactor Inspector

J. F. Drake, Senior Reactor Inspector

D. Loveless, Senior Reactor Analyst

C. A. Peabody, Resident Inspector

S. M. Alferink, Reactor Inspector

P. A. Jayroe, Project Engineer

C. Cauffman, Operations Engineer

A. L. Fairbanks, Reactor Inspector

C. C. Alldredge, Project Engineer

G. M. Vasquez, Senior Health Physicist

D. C. Graves, Health Physicist

Approved By:

G. B. Miller, Chief, Project Branch B

Division of Reactor Projects

- 2 -

Enclosure 2

SUMMARY OF FINDINGS

IR 05000482/2008005, 10/01/2009 - 12/31/2009; Wolf Creek Generating Station, Integrated

Resident and Regional Report; Fire Protection, Inservice Inspection Activities; Maintenance Risk

Assessments and Emergent Work Controls; Operability Evaluations; Plant Modifications;

Refueling Outage and Other Outage Activities; Radiation Safety; Identification and Resolution of

Problems, and Other Activities.

The report covered a 3-month period of inspection by resident inspectors and an announced

baseline inspections by a regional based inspectors. Fourteen Green and one Severity Level IV

noncited violation were identified and two Green cited violations were also identified. The

significance of most findings is indicated by their color (Green, White, Yellow, or Red) using

Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the

significance determination process does not apply may be Green or be assigned a severity level

after NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

A.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors identified a noncited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, involving the licensees failure to

identify sources of boron leakage and document them in a corrective action document.

Specifically, prior to October 23, 2009, the licensee failed to accomplish the

requirements of Procedure AP 16F-001, Boric Acid Corrosion Control Program,

Revision 5, step 6.4.1, which states, in part, Sources of boron seepage/leakage shall

be identified/verified and documented in the applicable corrective action document.

During a boric acid walkdown, the inspectors identified 11 sources of boron leakage

which had not been previously identified and documented by the licensee. The licensee

entered this finding into their corrective action system as Condition Report 00021274.

The finding was determined to be more than minor because it was associated with the

Initiating Events Cornerstone attribute of human performance and affected the

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. The

inspectors used Inspection Manual Chapter 0609, Significance Determination Process,

Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, and

determined the finding was of very low safety significance (Green) because the issue

would not result in exceeding the technical specification limit for identified reactor

coolant system leakage or affect other mitigating systems resulting in a total loss of their

safety function. The inspectors also determined that the finding had a crosscutting

aspect in the area of problem identification and resolution, operating experience, where

the licensee did not institutionalize operating experience through changes to station

processes, procedures, equipment, and training programs [P.2.(b)] (Section 1R08.2.b).

- 3 -

Enclosure 2

Green. On December 16, 2009, inspectors identified a noncited violation of 10 CFR

Part 50, Appendix B, Criterion III, Design Control, involving failure to obtain vendor

design data for a modification. In August 2009, a component cooling water modification

was made to the reactor coolant pump thermal barrier heat exchangers flow rates as a

corrective action to VIO 05000482/2009002 07 (EA-09-110). A flow rate above the

previous design value was justified by an internal memo of a vendor opinion from a

telephone conversation in 1992. The inspectors found this to be contrary to

Procedure AP 05-005, for obtaining data from vendors. The notice of violation will

remain open until full compliance has been restored. Wolf Creek consulted with

Westinghouse, confirmed the acceptability of the increased flow rate, and requested a

formal calculation. This issue is captured in Condition Report 22824.

The inspectors determined that this finding was more than minor because this issue

aligned with Inspection Manual Chapter 0612, Appendix E, example 2.f, in that the

modification relied on verbal statements to raise the allowable flow through the heat

exchanger. This is a significant deficiency in the modification package. The inspectors

determined this finding was associated with the design control attribute of the Initiating

Events Cornerstone and affected the cornerstone objective to limit the likelihood of

events that upset plant stability and challenge critical safety functions. The inspectors

evaluated the significance of this finding using Phase 1 of Inspection Manual

Chapter 0609.04 and determined that the finding was of very low safety significance

because assuming worst case degradation, the finding would not result in exceeding the

technical specification limit for identified reactor coolant system leakage and would not

have likely affected other mitigation systems resulting in a total loss of their safety

function because seal injection was available. This finding has a crosscutting aspect in

the area of human performance associated with work practices in that management was

unsuccessful in communicating expectations on procedure use and adherence in

engineering H.4.b] (Section 1R18).

Green. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, due to an inadequate vent path for the reactor vessel

head. The inadequate vent path resulted in the formation of voids in the reactor vessel

head during Refueling Outage 17. Failure to ensure an adequate vent path in the

reactor vessel head was the subject of a noncited violation in NRC Inspection

Report 05000482/2008004. During and after Refueling Outage 16, Wolf Creek initiated

a root cause evaluation and corrective actions to prevent occurrence. When one of the

possible root causes was disproven in Refueling Outage 17, no additional action was

taken to determine the cause of the vessel head vent blockage. However, the licensee

could not exclude blockage in the piping. This issue was entered into the corrective

action program and the licensee plans to conduct a more thorough inspection of the

piping during the next refueling outage. This issue is being tracked by the licensee as

Condition Report 22501.

The inspectors determined that the failure to provide adequate vessel head vent path to

prevent gas accumulation in the reactor vessel during depressurized plant operations

was a performance deficiency. The inspectors determined that this finding, which was

associated with the Initiating Events Cornerstone, was more than minor because if left

uncorrected, it would have become a more significant-safety concern. Specifically,

- 4 -

Enclosure 2

without an adequate vent path the reactor vessel does not have an effective means of

relieving noncondensable gases to prevent a loss of reactor coolant system inventory.

The inspectors evaluated this finding using Inspection Manual Chapter 0609,

Appendix G, Attachment 1, and determined it be of very low safety significance based

upon the demonstrated availability of mitigating systems and the flooded reactor cavity

inventory. The inspectors determined the cause of the finding had a problem

identification and resolution aspect in the corrective action program. Specifically, Wolf

Creeks corrective actions were not successful to address the vent path blockage in a

timely manner P.1(d) (Section 1R20).

Green. The inspectors identified a noncited violation of License Condition 2.C.(5), Fire

Protection, for the failure to implement and maintain the approved fire protection

program. Specifically, the licensee prescribed mitigating actions in response to certain

fire scenarios that would result in a loss of circuit breaker coordination and could initiate

secondary fires in plant locations outside of the initial fire area. The licensee entered

this issue into their corrective action program as Condition Report 2008-005210.

This finding was more than minor because it was associated with the Protection Against

External Factors attribute of the Initiating Events Cornerstone and adversely affected the

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during shutdown as well as power operations. The

risk significance of this finding was determined using Manual Chapter 0609, Appendix F,

Fire Protection Significance Determination Process. The finding was determined to be

of very low safety significance using a Phase 2 evaluation. This finding was not

assigned a crosscutting aspect because the cause was not representative of current

performance (Section 4OA5.2).

Cornerstone: Mitigating Systems

Green. The inspectors identified a cited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, for failure to take action to stop leakage from the base

of the refueling water storage tank or evaluate the leakage and wastage for

acceptability. Specifically, the licensee did not take actions to prevent recurring

discolored boric acid deposits for approximately 11 years. Failure to correct leakage

from the refueling water storage tank base was the subject of a noncited violation in

NRC Inspection Report 05000482/2007006. This issue was entered into the licensee's

corrective action program as Condition Report 22866.

The failure to implement corrective actions for the refueling water storage tank leakage

was a performance deficiency. The inspectors determined this issue impacted the

Mitigating Systems Cornerstone and was greater than minor because if left uncorrected,

the failure to correct the presence of boric acid leakage could become a more significant

safety concern in that continued wastage could impact tank operability. Using the

Phase 1 worksheets in Inspection Manual Chapter 0609.04, "Significance Determination

Process," the finding was determined to have very low safety significance because it did

not result in a system or component being inoperable and it did not screen as potentially

risk significant due to a seismic, flooding, or severe weather initiating event. The

inspectors identified a crosscutting aspect in the area of human performance associated

- 5 -

Enclosure 2

with resources. Specifically, Wolf Creek did not maintain long-term plant safety

minimizing corrective maintenance deferrals and this long-standing equipment issue

H.2.c] (Section 1R05).

Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a,

for an inadequate Procedure AP-10-101, Control of Transient Ignition Sources. On

October 21, 2009, the inspectors observed maintenance personnel performing weld

preparation work on essential service water piping to containment cooler B using a

flapper wheel. The inspectors observed that the ignition control barriers for the hot work

were insufficient in that the sparks from the preparation work extended four to five feet

from the job site and there was no fire watch posted. On December 4, 2003, a

procedure revision inappropriately incorporated a change to the procedure where a fire

watch did not have to be posted when using wire brushes, flapper wheels, polishing

devices, or Rol-Lok type buffing pads mounted on power grinder motor drives or air

tools. The maintenance supervisor stopped the work until a fire watch was posted. The

licensee entered this into their corrective action system as Condition Report 20993.

This finding is more than minor because it affected the Mitigating Systems Cornerstone

attribute of Protection Against External Factors - Fires, and adversely affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences. The lack of a posted

fire watch could adversely affect the ability to achieve and maintain safe shutdown in the

event of a severe fire in the affected area. Inspection Manual Chapter 0609,

Appendix F, Fire Protection Significance Determination Process, could not be used to

effectively evaluate the finding and defense-in-depth strategies because the 2003

changes to the fire watch program affected multiple fire areas and conditions. Therefore,

in accordance with Inspection Manual Chapter 0609, Appendix M, the safety significance

was determined by regional management review who concluded that the finding was of

very low safety significance (Green). This finding was reviewed for crosscutting aspects

and none were identified. The original change occurred in 2003 and was not indicative

of current performance (Section 1R05.2).

Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(4) involving the

failure to adequately perform shutdown risk assessments during Refueling Outage 17.

Between October 10 and November 17, 2009, Wolf Creek did not appropriately consider

electrical power, decay heat removal, and containment when assessing shutdown risk.

This changed the outcome or color of the qualitative calculation on several occasions.

The licensee entered this issue in their corrective action program as Condition

Reports 22295 and 22296.

The failure to meet shutdown risk assessment requirements in the daily shutdown risk

assessment process is a performance deficiency. The inspectors determined this finding

was associated with the Mitigating Systems Cornerstone and was more than minor

because it involved incorrect risk assessment assumptions by omitting requirements

specified in committed guidance without providing justification for that omission. Such

errors of omission have the potential to change the outcome of the licensees

maintenance risk assessment as described above. Per Inspection Manual

- 6 -

Enclosure 2

Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management

Significance Determination Process, licensees who only perform qualitative analyses of

plant configuration risk due to maintenance activities, the significance of the deficiencies

must be determined by an internal NRC management review using risk insights where

possible in accordance with Inspection Manual Chapter 612, Power Reactor Inspection

Reports. The NRC management review concluded that this finding was of Green safety

significance because missing risk management actions did not result in loss of key

shutdown risk functions. Additionally, the cause of the finding has a human performance

crosscutting aspect in the area associated with the resources. Specifically, Wolf Creek

did not ensure that Procedure APF 22B-001-02 was complete, accurate, and up-to-date

H.2(c) (Section 1R13).

Green. On November 18, 2009, the inspectors identified a noncited violation of

Technical Specification 3.0.4.b for ascension from Mode 4 to Mode 3 without establishing

required risk management actions. Wolf Creek used technical specification Limiting

Condition for Operation 3.0.4.b to permit mode ascension after performance of a risk

assessment and identification of risk management actions to maintain safety in the next

mode. The turbine-driven auxiliary feedwater pump was inoperable per Technical

Specification 3.7.5. As a risk management action, protected train signs would be placed

on the doors to the motor-driven auxiliary feedwater Pump A and B room doors. A

walkdown conducted by the inspector on the morning of November 18, 2009, found that

the protected train signs on the motor-driven auxiliary feedwater pump rooms were not in

place. Also, a maintenance crew was performing radiography in the motor-driven

auxiliary feedwater pump Room B. The motor-driven auxiliary feedwater Pumps A and B

were also made inoperable (at separate times) later on the morning of November 18,

2009. The licensee entered this issue in their corrective action program as Condition

Report 21926.

Mode ascension under Technical Specification LCO 3.0.4.b without establishing required

risk management actions is a performance deficiency. The finding was more than minor

because it was associated with the configuration control and alignment attribute of the

Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. The configuration control issues not only included

the work being completed on the turbine-driven auxiliary feedwater pump, but also

included containment isolation valve testing and radiography that was performed on the

motor-driven auxiliary feedwater pumps which was not included in the risk assessment.

The inspector used Inspection Manual Chapter 0609.04, to determine that the finding

was of very-low safety significance (Green) because it did not result in a loss of system

safety function; did not exceed allowable technical specification outage time; and was

not a seismic, flooding, or severe weather concern. Additionally, the cause of the finding

has a human performance crosscutting aspect in the area associated with decision

making. Specifically, Wolf Creek used a risk assessment form and an informal mode

change form to communicate between departments the requirement for risk

management actions. The two forms were in conflict and the personnel who

implemented the risk management actions were not informed H.1(c) (Section 1R13).

- 7 -

Enclosure 2

Green. On October 15, 2009, the inspectors identified a noncited violation of 10 CFR

Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to

follow Procedure AP 28A-100, Condition Reports. Wolf Creek failed to initiate a

condition report for evaluation of corrosion on containment cooler A piping. After

inspector challenging, Wolf Creek initiated condition reports, performed nondestructive

testing, replaced corroded studs, and evaluated the cause of the corrosion.

The inspectors determined that the failure to follow AP 28A-100, Appendix C, was a

performance deficiency. This issue was more than minor because it was associated

with the equipment performance attribute of the Mitigating Systems Cornerstone and

affected the cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. Using

Inspection Manual Chapter 0609.04, the issue screened to Green because there was

not a loss of operability and the finding did not screen as potentially risk significant due

to a seismic, flooding, or severe weather initiating event. A crosscutting aspect was

identified in the problem identification and resolution area of the corrective action

program. Specifically, Wolf Creek failed to implement a corrective action program with a

low threshold for identifying issues P.1.a] (Section 1R13).

Green. On November 23, 2009, a self-revealing violation of Technical

Specification 5.4.1.a was identified when a technician failed to follow procedure and

emptied 45 gallons of oil from centrifugal charging Pump A rendering the pump

inoperable. The technician was supposed to remove the temperature indicator for

calibration but instead removed the thermowell which breached the lube oil subsystem

of centrifugal charging Pump A. An unplanned entry into Technical Specification 3.5.2,

Condition A, was made for approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. The licensee entered this issue in

their corrective action program as Condition Report 21993.

The failure to follow station procedures and correctly remove the detector was a

performance deficiency. The finding was more than minor because it was associated

with the equipment performance attribute of the Mitigating Systems Cornerstone and

affected the cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. The

inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual

Chapter 0609.04, and determined that the finding was of very low safety significance

(Green) because the pump was inoperable for less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Also, the finding did

not screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The inspectors identified a human performance crosscutting in the area

of work practices because self-checking and communication with the supervisor failed to

prevent the event H.4.a] (Section 1R13).

Green. On November 5, 2009, inspectors identified a noncited violation of 10 CFR

Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure

to perform an adequate operability evaluation required by procedure. The inspectors

identified that Operability Evaluation EF 09-010, Revisions 0 and 1, did not demonstrate

that the essential service water pumps could withstand a safe shutdown earthquake.

Revision 2 of the operability evaluation included calculations to demonstrate acceptable

- 8 -

Enclosure 2

stresses and included pump impeller clearances. This issue is captured in the corrective

action program as condition reports 22798 and 21572.

The failure to perform an adequate operability evaluation per Procedures AP 28-001

and AP 26C 004 was a performance deficiency. The inspectors determined that this

finding was more than minor because it is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone, and it affected the cornerstone objective

to ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences (i.e., core damage). Specifically, this issue

relates to the availability and reliability examples of the equipment performance attribute

because a latent common mode failure mechanism was not correctly evaluated. The

inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual

Chapter 0609, Appendix A, and determined that the finding was of very low safety

significance (Green) because the issue was not a design or qualification deficiency

confirmed to result in loss of operability or functionality, did not represent a loss of

system safety function, an actual loss of safety function of a single train for greater than

its technical specification allowed outage time, an actual loss of safety function of a

nontechnical specification risk-significant equipment train, and did not screen as

potentially risk significant due to a seismic, flooding, or severe weather initiating event.

The cause of the finding has a problem identification and resolution crosscutting aspect

associated with the corrective action program because Wolf Creek failed to thoroughly

evaluate the failure mechanism such that the resolutions address the causes and extent

of conditions, as necessary P.1.c] (Section 1R15).

Green. The inspectors identified a noncited violation of Technical Specification 5.4.1.a

for failure to properly implement Procedure AP 14A-003, Scaffold Construction and

Use, when scaffolding was erected against operable safety-related equipment. On

October 15, 2009, the inspectors walked down containment and identified scaffolding in

contact with component cooling water piping. The tag on the scaffold explicitly stated

that it was not seismically qualified. At the time, both steam generators were inoperable

and both trains of residual heat removal were required to be operable. The inspectors

reviewed the bases for Technical Specification 3.4.7, RCS Loops - Mode 5, Loops

Filled, which required an operable heat sink path from residual heat removal to

component cooling water to essential service water. This issue was entered into the

corrective action program as Condition Report 22464.

The construction of an unqualified scaffold against operable component cooling water

piping was a performance deficiency. The inspectors determined that this finding was

more than minor because it is associated with the equipment performance attribute for

the Mitigating Systems Cornerstone and affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). Specifically, this issue relates to

the availability and reliability examples of the equipment performance attribute because

a latent failure mechanism was not evaluated. The inspectors evaluated the significance

of this finding using Inspection Manual Chapter 0609, Appendix G, Attachment 1,

Shutdown Operations Significance Determination Process Phase 1 Operational

Checklists for Both PWRs and BWRs. The inspectors determined that Checklist 3 was

applicable because the unit was in cold shutdown with the refueling cavity level less than

- 9 -

Enclosure 2

23 feet. Using Appendix G, Attachment 1, Checklist 3, Phase 2 analysis was not

needed and the finding was of very low safety significance (Green) because the licensee

was able to demonstrate that the seismically unqualified scaffolding would not have

resulted in a loss of safety function. The inspectors determined the cause of the finding

had a human performance aspect in the area of resources. Specifically,

Procedure AP 14A-003 was inadequate because it had conflicting guidance that allowed

seismically unqualified scaffolds in Modes 5 and 6 H.2.c] (Section 1R20).

Cornerstone: Barrier Integrity

Green. The inspectors identified a noncited violation of Technical Specification 3.3.1,

Condition I, for making positive reactivity addition prohibited by technical specifications

in Mode 2 because one source range nuclear instrument channel was inoperable.

Following a reactor transient, one of the source range nuclear instrument channels

experienced an unanticipated increased count rate and was declared inoperable. Wolf

Creek restored the channel in an operability evaluation which cited the cause as a

problem in a component which was later determined not to exist in the installed

configuration; however, the improperly restored equipment had already been used for to

support plant startup on August 22, 2009. Wolf Creek replaced the detector during

Refueling Outage 17. This issue was entered into the correction action program as

Condition Report 20208.

Reactivity addition with source range channel Nuclear Instrument-31 inoperable is a

performance deficiency. The finding was more than minor because it was associated

with the configuration control (reactivity control) attribute of the Barrier Integrity

Cornerstone, and it affected the cornerstone objective to provide reasonable assurance

that physical design barriers (fuel cladding, reactor coolant system, and containment)

protect the public from radionuclide releases caused by accidents or events. The

inspectors evaluated the significance of this finding using Phase 1 of Inspection Manual

Chapter 0609.04, and determined that the finding screened to Green because the

finding only affected the fuel barrier. Additionally, the cause of the finding has a human

performance crosscutting aspect in the area associated with the decision making.

Specifically, Wolf Creek did not use conservative assumptions in decision making and

adopt requirements to demonstrate that the proposed action is safe in order to proceed

rather than a requirement to demonstrate that it is unsafe in order to disapprove the

action, when performing an operability evaluation for the source range Nuclear

Instrument 31 detector prior to restarting from a forced outage H.1(b) (Section 1R15).

Green. On December 30, 2009, the inspectors identified a noncited violation of

Technical Specification Table 3.3.1-1, Function 18.a, when Wolf Creek restarted on

May 18, 2005. During a reactor shutdown on October 7, 2006, intermediate range

neutron detector Nuclear Instrument-36 did not decrease below 6E -11 amps and

energize source range detector Nuclear Instrument-32. The detector was not replaced

until Refueling Outage 16 in March 2008. The licensee entered this issue in their

corrective action program as Condition Report 22450

The inspectors determined that the failure to ensure that the P-6 interlock was operable

per the technical specification as defined in the bases was a performance deficiency.

- 10 -

Enclosure 2

The finding was more than minor because it was associated with the configuration

control (reactivity control) attribute of the Barrier Integrity Cornerstone, and it affected the

cornerstone objective to provide reasonable assurance that physical design barriers (fuel

cladding, reactor coolant system, and containment) protect the public from radionuclide

releases caused by accidents or events. The inspectors evaluated the significance of

this finding using Phase 1 of Inspection Manual Chapter 0609.04, and determined that

the finding screened to Green because the P-6 interlock only affected the fuel barrier

(Section 4OA2). This finding was not assigned a crosscutting aspect because the cause

was not representative of current performance.

Cornerstone: Occupational Radiation Safety

Green. The inspector identified a noncited violation of Technical Specification 5.7.2.a.1

for failure to maintain administrative control of door and gate keys to high radiation areas

with dose rates greater than 1 rem per hour but less than 500 rads per hour (referred to

as locked high radiation areas). Specifically, as of October 21, 2009, the licensee did

not have administrative controls over a single master key to locked high radiation areas.

This issue was entered into the licensees corrective action program as Condition

Report 20973.

Failure to maintain administrative control of the master key to locked high radiation areas

was a performance deficiency. This finding is greater than minor because if left uncorrected

the finding has the potential to lead to a more significant safety concern in that an individual

could receive unanticipated radiation dose by gaining access a locked high radiation area

without the proper controls and briefing. This finding was evaluated using the occupational

radiation safety significance determination process and determined to be of very low safety

significance because it did not involve: (1) as low as is reasonably achievable planning or

work control issue, (2) an overexposure, (3) a substantial potential for overexposure, or

(4) an impaired ability to assess dose. Additionally, the violation has a crosscutting aspect

in the area of human performance associated with the work practices component because

the lack of peer and self-checking resulted in inadequate control of keys to locked high

radiation areas H.4(a) (Section 2OS1).

Cornerstone: Miscellaneous

Severity Level IV. The inspectors identified a Severity Level IV noncited violation of

10 CFR 50.73 in which the licensee failed to submit a licensee event report within 60 days

following discovery of events or conditions meeting the reportability criteria. On December

31, 2009, the inspectors identified a licensee event report that was no timely. Licensee

Event Report 2009-009-00 was not issued within 60 days for a condition prohibited by

technical specifications, and the event report did not identify that the disabling of both trains

of the P-4 interlock on August 22, 2009 was also reportable per 10 CFR 50.73(a)(2)(v). The

P-4 interlock was required by Technical Specification 3.3.2, function 8.a, and is discussed in

USAR, Section 7.3.8, NSSS Engineered Safety Feature Actuation System. Wolf Creek

licensee event report 2009-009 was correct in that the interlock is not credited in accident

analysis. However, NUREG 1022, Section 3.2.6, specifies that inoperable systems required

by the technical specifications be reported, even if there are other diverse operable means

of accomplishing the safety function.

- 11 -

Enclosure 2

The inspectors reviewed this issue in accordance with Inspection Manual Chapter 0612 and

the NRC Enforcement Manual. Through this review, the inspectors determined that

traditional enforcement was applicable to this issue because the NRC's regulatory ability

was affected. Specifically, the NRC relies on the licensee to identify and report conditions or

events meeting the criteria specified in regulations in order to perform its regulatory function,

and when this is not done, the regulatory function is impacted. The inspectors determined

that this finding was not suitable for evaluation using the significance determination process,

and as such, was evaluated in accordance with the NRC Enforcement Policy. The finding

was reviewed by NRC management, and because the violation was determined to be of

very low safety significance, was not repetitive or willful, and was entered into the corrective

action program, this violation is being treated as a Severity Level IV noncited violation

consistent with the NRC Enforcement Policy. This finding was determined to have a

crosscutting aspect in the area of problem identification and resolution associated with the

corrective action program in that the licensee failed to appropriately and thoroughly evaluate

for reportability aspects all factors and time frames associated with the inoperability of the

engineered safety features actuation system P.1(c) (Section 4OA3).

B.

Licensee-Identified Violations

Two violations of very low safety significance, which were identified by the licensee,

have been reviewed by the inspectors. Corrective actions taken or planned by the

licensee have been entered into the licensees corrective action program. These

violations and corrective action tracking numbers (condition report numbers) are listed in

Section 4OA7.

- 12 -

Enclosure 2

REPORT DETAILS

Summary of Plant Status

The plant started the inspection period at 100 percent rated thermal power. On October 10,

2009, Wolf Creek shutdown for Refueling Outage 17. On November 17, 2009, Wolf Creek

achieved criticality and on November 24, 2009, Wolf Creek achieved 100 percent power and

remained there for the remainder of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency

Preparedness

1R01 Adverse Weather Protection (71111.01)

.1

Readiness to Cope with External Flooding

a.

Inspection Scope

On October 28, 2009, the inspectors evaluated the design, material condition, and

procedures for coping with the design basis probable maximum flood. The evaluation

included a review to check for deviations from the descriptions provided in the Updated

Safety Analysis Report (USAR) for features intended to mitigate the potential for

flooding from external factors. As part of this evaluation, the inspectors checked for

obstructions that could prevent draining, checked that the roofs did not contain obvious

loose items that could clog drains in the event of heavy precipitation, and determined

that barriers required to mitigate the flood were in place and operable. Additionally, the

inspectors performed a walkdown of the protected area to identify any modification to

the site that would inhibit site drainage during a probable maximum precipitation event

or allow water ingress past a barrier. The inspectors also reviewed the abnormal

operating procedure for mitigating the design basis flood to ensure it could be

implemented as written.

These activities constitute completion of one external flooding sample as defined in

Inspection Procedure IP 71111.01-05.

b.

Findings

No findings of significance were identified.

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Enclosure 2

1R04 Equipment Alignments (71111.04)

.1

Partial Walkdown

a.

Inspection Scope

The inspectors performed partial walkdown of the following risk-significant systems:

October 21, 2009, Train A while emergency diesel generator B and offsite power

out of service for maintenance

October 21, 2009, Spent fuel pool train A while spent fuel pool train B out of

service

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating Procedures,

system diagrams, USAR, technical specification requirements, administrative technical

specifications, outstanding work orders, condition reports, and the impact of ongoing

work activities on redundant trains of equipment in order to identify conditions that could

have rendered the systems incapable of performing their intended functions. The

inspectors also walked down accessible portions of the systems to verify system

components and support equipment were aligned correctly and operable. The

inspectors examined the material condition of the components and observed operating

parameters of equipment to verify that there were no obvious deficiencies. The

inspectors also verified that the licensee had properly identified and resolved equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers and entered them into the corrective action program with

the appropriate significance characterization. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of two partial system walkdown samples as

defined in Inspection Procedure IP 71111.04-05.

b.

Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1

Quarterly Fire Inspection Tours

a.

Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

- 14 -

Enclosure 2

October 7, 2009, Auxiliary boiler oil combustion Impact on turbine-driven auxiliary

feedwater room

October 29, 2009, Spent fuel pool Room A

October 15, 2009, All levels of containment in Mode 5

November 12, 2009, Refueling water storage tank valve house

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants individual plant examination of external events with later

additional insights, their potential to affect equipment that could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples

as defined by Inspection Procedure IP 71111.05-05.

b.

Findings

.1

Failure to Correct Discolored Boric Acid Deposits

Introduction. The inspectors identified a Green cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for the failure to take action to stop

leakage from the base of the refueling water storage tank or evaluate the leakage and

wastage for acceptability.

Description. During the component design basis inspection in June 2007, the inspection

team noted white and brown deposits resembling boric acid at the base of the refueling

water storage tank. The licensee informed the team that past analysis had determined

these deposits were from calcium-silicate insulation which had been used for insulating

the refueling water storage tank. In 1998, the licensee had initiated Problem

Identification Request 1998-3860 to pursue the nature of the deposits and discovered

that the deposits did contain amounts of insulation, but also contained boron. The

licensee had dismissed the boron as spillage from a sampling evolution. On two

subsequent occasions after 1998, the deposits were questioned by the licensee and

- 15 -

Enclosure 2

again dismissed as insulation based on the 1998 resolution. In each of these cases the

deposits were cleaned up, and the problem identification requests written only

addressed the poor materiel condition of the area. The component design basis

inspection team questioned the previous conclusions that the deposits were insulation

material based on the strong resemblance to boric acid deposits from leakage of reactor

coolant from the refueling water storage tank. The licensee sent samples of the deposits

for offsite laboratory analysis, which confirmed that the deposits contained boron.

Subsequently, the licensee performed inspections of the carbon steel components in the

area and determined that no significant wastage had occurred and operability of the

refueling water storage tank and its surrounding components was not affected. The

inspection team documented a noncited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, for inadequate corrective actions in response to the leakage from the

refueling water storage tank, documented in NRC Inspection Report 05000482/2007006

(ADAMS ML072880678)

On November 12, 2009, the resident inspectors walked down the refueling water storage

tank valve house and again identified that the base of the refueling water storage tank

had deposits that resembled boric acid in several locations. Some deposits had

progressed up the tank bolting several inches from the floor. Initially, Wolf Creek again

maintained that the deposits were calcium silicate from insulation. The inspectors

questioned the licensee about the deposits, and laboratory testing again demonstrated

the presence of boric acid.

The inspectors reviewed the actions Wolf Creek had taken in response to NCV

05000482/2007006-03 in the component design basis inspection report. Wolf Creek had

performed a boric acid corrosion evaluation as part of Work Order 07-300734-000, which

concluded that the refueling water storage tank leak was not active, though the tank

deposits reappeared after cleanings in July 2007, August 2008, March 2009, June 2009,

and September 2009. Wolf Creek attempted to repair roof leaks in the refueling water

storage tank valve house as a source of rain water ingress, but took no action to address

the source of the boric acid in the deposits. Wolf Creek took several samples of

deposits from the base of the refueling tank. Though one sample in June 2009 did not

contain boric acid, the majority of samples, including the most recent sample from

November 2009, did contain boron, indicating that leakage from the base of the refueling

water storage tank continued to exist. The inspectors concluded that Wolf Creek had

failed to restore compliance from the noncited violation involving the failure to correct

refueling water storage tank leakage in the component design basis inspection report.

Analysis. The failure to implement corrective actions for the refueling water storage tank

leakage was a performance deficiency. Traditional enforcement does not apply since

there were no actual safety consequences or potential for impacting the NRC's

regulatory function, and the finding was not the result of any willful violation of NRC

requirements or Wolf Creek procedures. The issue was greater than minor because if

left uncorrected, the failure to correct the presence of boric acid for extended periods of

time would become a more significant-safety concern, in that, continued wastage could

impact the studs and tank operability. The finding affected the Mitigating Systems

Cornerstone, using the Phase 1 worksheets in Inspection Manual Chapter 0609.04,

"Significance Determination Process." The inspectors determined that the finding had

- 16 -

Enclosure 2

very low safety significance (Green) because it did not result in a system or component

being inoperable and it did not screen as potentially risk significant due to a seismic,

flooding, or severe weather initiating event. The inspectors identified a crosscutting

aspect in the area of human performance associated with resources. Specifically, Wolf

Creek did not maintain long-term plant safety minimizing corrective maintenance

deferrals and this long-standing equipment issue H.2(c).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

requires, in part, that measures shall be established to assure that conditions adverse to

quality are promptly identified and corrected. Contrary to the above, from 1998 to

December 31, 2009, Wolf Creek did not correct the condition adverse to quality.

Specifically, Wolf Creek did not take action to correct leakage from the refueling water

storage tank. This issue and the corrective actions are being tracked in Condition

Reports 2007-02742 and 22866. Due to the licensees failure to restore compliance

from previous NCV 05000482/2007006-03 within a reasonable time after the violation

was identified, this violation is being cited as a Notice of Violation consistent with Section

VI.A of the Enforcement Policy: VIO 05000482/2009005-01, Failure to Correct

Discolored Boric Acid Deposits (EA-10-004).

.2

Control of Transient Ignition Sources

Introduction. The inspectors identified a noncited violation of Technical

Specification 5.4.1.a for an inadequate procedure for control of transient ignition sources

due to exempting the use of flapper wheels from the requirements of AP 10-101,

Control of Transient Ignition Sources.

Description. On October 21, 2009, NRC inspectors observed maintenance personnel

performing weld preparation work on essential service water piping to containment

cooler B. The inspectors observed that the ignition control barriers for the hot work were

insufficient, in that the sparks from the preparation work extended four to five feet from

the job site and there was no fire watch apparent. When the inspectors questioned the

maintenance personnel regarding the posting of a fire watch, the maintenance personnel

stated that they were using a flapper wheel and a fire watch was not required.

On December 4, 2003, the licensee modified Procedure AP-10-101, Control of

Transient Ignition Sources, such that the use of flapper wheels was exempted from the

requirements of Procedure AP10-101. The inspectors determined that the revised

procedure adversely affected the fire safety in the affected area. This was based on

recognition that the ability of the fire watch was not limited to fire identification in a timely

manner, but also on mitigation actions that an established fire watch could take in the

event of fires. These could include such actions as the ability to close doors limiting fire

exposure to adjacent areas and providing more timely fire detection capability in certain

cases. The inspectors concluded that the licensee inappropriately revised the procedure

to exempt the use of all flapper wheels without posting a fire watch. The inspectors

determined that the inadequate procedure increased the risk of fires in the plant.

Analysis. The licensee's failure to provide an adequate procedure to control transient

ignition sources was a performance deficiency and was reasonably within the ability of

- 17 -

Enclosure 2

the licensee to prevent. The inspectors concluded that this issue had a realistic

likelihood of affecting safety. Failure to properly evaluate the removal of the fire watch

posting requirements could adversely affect or degrade the ability of the licensee to

identify and report fires caused by hot work, in a timely manner. Specifically, the use of

nonconservative exemptions for requiring fire watches to be posted could affect the

ability to adequately reduce the risk of fires in the plant. This finding is more than minor

because it affected the Mitigating Systems Cornerstone attribute of Protection Against

External Factors - Fires, and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. The lack of a posted fire watch could adversely

affect the ability to achieve and maintain safe shutdown in the event of a severe fire in

the affected area. Inspection Manual Chapter 0609, Appendix F, Fire Protection

Significance Determination Process, could not be used to effectively evaluate the

finding in relation to defense-in-depth strategies because it had potential effects across

multiple areas and conditions. Therefore, in accordance with Inspection Manual

Chapter 0609, Appendix M, the safety significance was determined by regional

management review and concluded that the finding was of very low safety significance

(Green) since there were no combustibles in the immediate area and fire extinguishers

were readily available. The capability of other principal defense-in-depth fire protection

features were unaffected, such as the associated fire barriers, control of transient

combustibles, manual fire suppression equipment, and the fire brigade. Additionally, the

finding was not associated with a qualification deficiency, did not result in a loss of safety

function for a system, and was not risk significance due to external initiating events.

Enforcement. Technical Specification 5.4.1.a requires, in part, that written procedures

shall be established and maintained covering the applicable procedures recommended

in Regulatory Guide 1.33, Revision 2, Appendix A, February 1972. Regulatory

Guide 1.33, "Quality Assurance Program Requirements (Operation)," Revision 2,

Appendix A, Section 1.l, requires that procedures be written for plant fire protection

program. Contrary to this requirement, from December 4, 2003, until October 21, 2009,

the licensee inappropriately exempted the use of flapper wheels from the requirements

of Procedure AP 10-101, Control of Transient Ignition Sources, reducing the fire safety

of the plant. Because this issue was determined to be of very low safety significance

(Green) and was entered into the licensees corrective action program as Condition

Report AR 00020993, this violation is being treated as a noncited violation in accordance

with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2009005-02,

Control of Transient Ignition Sources.

1R06 Flood Protection Measures (71111.06)

a.

Inspection Scope

The inspectors reviewed the USAR, the flooding analysis, and plant procedures to

assess seasonal susceptibilities involving internal flooding; reviewed the USAR and

corrective action program to determine if licensee personnel identified and corrected

flooding problems; inspected underground bunkers/manholes to verify the adequacy of

sump pumps, level alarm circuits, cable splices subject to submergence, and drainage

- 18 -

Enclosure 2

for bunkers/manholes; verified that operator actions for coping with flooding can

reasonably achieve the desired outcomes; and walked down the area listed below to

verify the adequacy of equipment seals located below the flood line, floor and wall

penetration seals, watertight door seals, common drain lines and sumps, sump pumps,

level alarms, and control circuits, and temporary or removable flood barriers. Specific

documents reviewed during this inspection are listed in the attachment.

October 6, 2009, Auxiliary feedwater rooms and sump pumps

These activities constitute completion of one flood protection measures inspection

sample as defined by Inspection Procedure IP 71111.06-05.

b.

Findings

No findings of significance were identified.

1R07 Heat Sink Performance (71111.07)

.1

Annual Inspection

a.

Inspection Scope

The inspectors reviewed licensee programs, verified performance against industry

standards, and reviewed critical operating parameters and maintenance records.

January 14, 2009, STN PE-38 on containment cooler SGN01D

The inspectors verified that performance tests were satisfactorily conducted for heat

exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the

periodic maintenance method outlined in Electric Power Research Institute

Report NP 7552, "Heat Exchanger Performance Monitoring Guidelines;" the licensee

properly utilized biofouling controls; the licensees heat exchanger inspections

adequately assessed the state of cleanliness of their tubes; and the heat exchanger was

correctly categorized under 10 CFR 50.65, Requirements for Monitoring the

Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed

during this inspection are listed in the attachment.

These activities constitute completion of one heat sink inspection sample as defined by

Inspection Procedure IP 71111.07-05.

b.

Findings

No findings of significance were identified.

- 19 -

Enclosure 2

1R08 Inservice Inspection Activities (71111.08)

.1

Inspection Activities Other Than Steam Generator Tube Inspection, Pressurized Water

Reactor Vessel Upper Head Penetration Inspections, Boric Acid Corrosion Control

(71111.08-02.01)

a.

Inspection Scope

The inspection procedure requires review of two or three types of nondestructive

examination activities and, if performed, one to three welds on the reactor coolant

system pressure boundary. It also requires review of one or two examinations with

relevant indications (if any were found) that have been accepted by the licensee for

continued service.

The inspectors directly observed the following nondestructive examinations:

SYSTEM

WELD IDENTIFICATION

EXAMINATION

TYPE

Feedwater System

Check Valve. Root pass indication

repair. Area 5, West Bay

Drawing WIP-M-13AE05-012-A-1

WO 08-305300-049

MT

Charging Pump

Room B

Vent valve. 1974 foot elevation

auxiliary building, Room 1108

Drawing WIP-M-13BG02-006-A-1

WO 08-310289-043

PT

Safety Injection

Vent Valve. Located in safety

injection pump Room A

Drawing WIP-M-13EM01-008-A-1

WO 0-310289-077

PT

Chemical and Volume

Control System

Blowdown line coupling letdown heat

exchanger room Drawing M-13BG34

WO 06-288993-000

PT

Feedwater System

Check valve hinge pin seal weld.

2047 foot elevation, RB C loop

Drawing WOP-M-13AE04-008-A-1

WO 08-305300-013

PT

- 20 -

Enclosure 2

SYSTEM

WELD IDENTIFICATION

EXAMINATION

TYPE

Feedwater System

Check valve - flange to pipe weld

joint. 2026 elevation of Area 5

WO 08-305300-048 and -049

RT

Reactor Vessel

Closure Head

RPV meridonal welds,

ISI Number CH-101-104-B

UT

Reactor Vessel

Closure Head

RPV meridonal weld,

ISI Number CH-101-104-C

UT

High Pressure Safety

Injection

HPSI pipe to elbow weld, ISI Number

EM-03-S015-B

UT

Residual Heat

Removal

Pipe to Pipe Weld,

ISI Number EJ-04-F019

UT

Reactor Vessel

Closure Head

Reactor vessel washer and

Bushings 19-24,

Component CH-WASH 19-24

Drawing M-189-50ISI-RBB01

WO 08-311169-014

VT - 1

Safety Injection

Vent valve. Safety injection pump

Room A

Drawing WIP-M-13EM01-008-A-01

WO 08-310289-068

VT - 1

Reactor Vessel Head

Required by 10FR50.55a, ASME

Code Case N-729-1. Also IEWA-2212

VT-2 under mirror insulation

WO 08-307175-001

VT - 2

Piping Support

In containment

Component EJ-04-H002

WO 08-311169-001

VT- 3

Piping Support

In containment.

Component EM-03-C033

WO 06-288978-001

VT- 3

- 21 -

Enclosure 2

SYSTEM

WELD IDENTIFICATION

EXAMINATION

TYPE

Piping Support

In containment.

Component BG-22-H007

WO 08-311169-011

VT- 3

During the review and observation of each examination, the inspectors verified that

activities were performed in accordance with ASME Boiler and Pressure Vessel Code

requirements and applicable procedures. During the observed nondestructive

examinations identified above, three relevant indications were identified (one dye

penetrant, one radiograph, and one boric acid leak on the control rod drive mechanism

canopy seal weld). Indications identified were dispositioned in accordance with ASME

Code and approved procedures. The two weld indications were removed and

re-examined. A control rod drive mechanism canopy seal weld clamp was installed.

There were no examinations performed where relevant indications had been accepted

by the licensee for continued service. The qualifications of all nondestructive

examination technicians performing the inspections were verified to be current.

The inspectors directly observed a portion of the following welding activities:

SYSTEM

WELD IDENTIFICATION

WELD TYPE

Reactor Coolant

Pump Seal

Water

Reactor coolant pump seal

water supply line drain.

1974 foot elevation auxiliary

building, letdown heat

exchanger room.

WO 06-288993-000.

Inlay, Gas Tungsten Arc

Welding, hand welded

High Pressure

Safety Injection

System

Vent valve. 1974 foot elevation

of auxiliary building, area 1.

WO 08-310289-077

Inlay, Gas Tungsten Arc

Welding, hand welded

Chemical and

Volume Control

System

Vent valve. Reactor water

storage tank to centrifugal

charging Pump A suction check

valve. 1974 foot elevation of

auxiliary building, area 1.

WO 08-310289-007

Inlay, Gas Tungsten Arc

Welding, hand welded

- 22 -

Enclosure 2

SYSTEM

WELD IDENTIFICATION

WELD TYPE

Essential

Service Water

System

Containment cooler B ESW

supply isolation valve (install

flanges on pipe for butterfly

valve). 2047 foot elevation in

containment, near Cooler B

duct. WO 07-299593-012.

Inlay, Gas Tungsten Arc

Welding, hand welded

Chemical and

Volume Control

System

Vent valve. Safety Injection

Pump Room B

Valves BG-V0842 and V0843.

1974 foot elevation of auxiliary

building, area 1.

WO 08-310289-043.

Inlay, Gas Tungsten Arc

Welding, hand welded

The inspectors verified, by review, that the welding procedure specifications and the

welders had been properly qualified in accordance with ASME Code,Section IX,

requirements. The inspectors also verified through record review that essential variables

for the welding process were identified, recorded in the procedure qualification record,

and formed the bases for qualification of the welding procedure specifications. Specific

documents reviewed during this inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 02.01 of Inspection

Procedure IP 71111.08.

b.

Findings:

A finding involving control of transient ignition sources is described in Section 1RO5.2 of

this report.

.2

Vessel Upper Head Penetration Inspection Activities (71111.08-02.02)

a.

Inspection Scope

The inspectors witnessed the licensees performance of the required visual inspection

(VT-2) of the reactor head and pressure-retaining components above the reactor

pressure vessel head in accordance with requirement of ASME Code Case N-729-1 as

mandated by 10 CFR 50.55a effective October 10, 2008. Implementation required

ASME Code IWA-2212 VT-2 under the mirror insulation on top of the reactor head

through multiple access points. The inspectors reviewed the results of this inspection for

evidence of leaks or boron deposits at reactor pressure boundaries and related

insulation above the head. Specific documents reviewed during this inspection are listed

in the attachment.

- 23 -

Enclosure 2

These actions constitute completion of the requirements for Section 02.02 of Inspection

Procedure PI 71111.08.

b.

Findings

No findings of significance were identified.

.3

Boric Acid Corrosion Control Inspection Activities (71111.08-02.03)

a.

Inspection Scope:

The inspectors evaluated the implementation of the licensees boric acid corrosion

control program for monitoring degradation of those systems that could be adversely

affected by boric acid corrosion. The inspection procedure required review of plant

areas that had recently received a boric acid walkdown by the licensee, through either

direct observation or record review. The inspectors reviewed the records associated with

the licensees most recent boric acid corrosion control walkdown, as specified in

Procedure STN PE-040D, "RCS Pressure Boundary Integrity Walkdown, Revision 3.

The inspectors directly observed some of those plant areas recently walked down by the

licensee. Additionally, the inspectors independently walked down piping and

components containing boric acid inside containment and the auxiliary building. The

inspection procedure also required verification that visual inspections emphasize

locations where boric acid leaks can cause degradation of safety-significant components.

The inspectors verified through record review that the boric acid corrosion control

inspection efforts were directed towards locations where boric acid leaks can cause

degradation of safety-related components.

The inspection procedure required review of one to three engineering evaluations

performed for boric acid found on reactor coolant system piping and components. For

those sources of boron leakage identified, the engineering evaluations gave assurance

that the ASME Code wall thickness limits were properly maintained. The inspection

procedure also required review of one to three corrective actions performed for evidence

of boric acid leaks identified. The inspectors confirmed that the work orders and

evaluations generated in response to boron leakage identification were consistent with

requirements of the ASME Code and 10 CFR Part 50, Appendix B, Criterion XVI.

Specific documents reviewed during this inspection are listed in the attachment.

These actions constitute completion of the requirements for Section 02.03 of Inspection

Procedure IP 71111.08

b.

Findings

Introduction. The inspectors identified a noncited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees

failure to identify sources of boron leakage and document them in a corrective action

document. Specifically, during a boric acid walkdown, the inspectors identified

- 24 -

Enclosure 2

11 sources of boron leakage which had not been previously identified and documented

by the licensee.

Description. On October 23, 2009, the inspectors performed a boric acid walkdown of

areas inside containment and the auxiliary building. The inspectors identified 11 sources

of leakage which had not been previously identified and documented in a corrective

action document by the licensee during the licensees boric acid walkdowns completed

on October 11, 2009. With the exception of one leak, the leaks were not active and only

had small amounts of boric acid crystals present.

The inspectors noted that those boron leakage sources which were identified during the

walkdown inside containment were described by the licensee in the completed

walkdown procedure as having no boron indication. The licensee stated that their boric

acid inspections were focused on larger amounts of boron leakage and may have been

insensitive to smaller amounts of leakage. This is contrary to station

Procedure AP 16F-001, "Boric Acid Corrosion Control Program," Revision 5, step 6.4.1,

which states that: Sources of boron seepage/leakage shall be identified/verified and

documented in the applicable corrective action document. The licensee entered the

missed leakage sources into their corrective action program and initiated a condition

report to follow up on the extent of condition of missed boron leakage sources.

Analysis. The inspectors determined that the failure to identify sources of boron leakage

was contrary to station procedures and was a performance deficiency. Specifically,

11 examples of boron leakage were not identified and documented in a corrective action

document.

The finding was determined to be more than minor in accordance with Inspection

Manual Chapter 0612, Appendix B, Issue Screening, because it was associated with

the human performance attribute of the Initiating Events Cornerstone and affected the

cornerstone objective of limiting the likelihood of those events that upset plant stability

and challenge critical safety functions during shutdown as well as power operations.

Specifically, boric acid leakage has historically been found to degrade carbon steel

components which could affect the reactor coolant system pressure boundary or impact

the reliability of emergency core cooling systems. The inspectors used Inspection

Manual Chapter 0609, Significance Determination Process, Attachment 4, Phase 1 -

Initial Screening and Characterization of Findings, and determined the finding was of

very low safety significance (Green) because the issue would not result in exceeding the

technical specification limit for identified reactor coolant system leakage or effect other

mitigating systems resulting in a total loss of their safety function. The inspectors also

determined that the finding had a crosscutting aspect in the area of problem

identification and resolution, operating experience, where the licensee did not

institutionalizes operating experience through changes to station processes, procedures,

equipment, and training programs [P.2.(b)].

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, states, in part, that Activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

- 25 -

Enclosure 2

circumstances and shall be accomplished in accordance with these instructions,

procedures, or drawings. Licensee Procedure AP 16F-001,"Boric Acid Corrosion

Control Program," Revision 5, which prescribes activities affecting quality, states, in part,

that sources of boron seepage/leakage shall be identified/verified and documented in

the applicable corrective action document. Contrary to the above, prior to October 23,

2009, the licensee failed to accomplish the requirements of Procedure AP 16F-001.

Specifically, the licensee failed to identify 11 sources of boron leakage in the containment

structure and the auxiliary building and document them in a corrective action document.

Because this issue was determined to be of very low safety significance (Green) and

was entered into the licensees corrective action program as Condition

Report AR-00021274, this violation is being treated as a noncited violation in accordance

with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000482/2009005-03,

Failure to Identify Sources of Boron Leakage.

.4

Steam Generator Tube Inspection Activities (71111.08-02.04)

a.

Inspection Scope:

The inspection procedure specified performance of an assessment of in situ screening

criteria to assure consistency between assumed nondestructive examination flaw sizing

accuracy and data from the EPRI examination technique specification sheets. It further

specified assessment of appropriateness of tubes selected for in situ pressure testing,

observation of in situ pressure testing, and review of in situ pressure test results.

At the time of this inspection, no conditions had been identified that warranted in situ

pressure testing. The inspectors reviewed the Licensees Report SG-CDME-08-15,

Wolf Creek Refueling 16 Condition Monitoring Assessment and Operational

Assessment, Revision 1, dated April 2008, and compared the in situ test screening

parameters to the guidelines contained in the EPRI document In Situ Pressure Test

Guidelines, Revision 2. This review determined that the remaining screening

parameters were consistent with the EPRI guidelines.

In addition, the inspectors reviewed both the licensee site-validated and qualified

acquisition and analysis technique sheets used during this refueling outage and the

qualifying EPRI examination technique specification sheets to verify that the essential

variables regarding flaw sizing accuracy, tubing, equipment, technique, and analysis had

been identified and qualified through demonstration. The inspector-reviewed acquisition

technique and analysis technique sheets are identified in the attachment.

The inspection procedure specified comparing the estimated size and number of tube

flaws detected during the current outage against the previous outage operational

assessment predictions to assess the licensees prediction capability. The inspectors

compared the previous outage operational assessment predictions contained in

Report SG-CDME-08-15, Revision 1, with the flaws identified thus far during the current

steam generator tube inspection effort. Compared to the projected damage

mechanisms identified by the licensee, the number of identified indications fell within the

range of prediction and was quite consistent with predictions.

- 26 -

Enclosure 2

The inspection procedure specified confirmation that the steam generator tube test

scope and expansion criteria meet technical specification requirements, EPRI

guidelines, and commitments made to the NRC. The inspectors evaluated the

recommended steam generator tube eddy current test scope established by technical

specification requirements. The inspectors compared the recommended test scope to

the actual test scope and found that the licensee had accounted for all known flaws and

had established a test scope that met or exceeded minimum technical specification

requirements, EPRI guidelines, and commitments made to the NRC. The scope of the

licensees Eddy current examinations of tubes in both steam generators included:

100 percent, bobbin examination of tubes in steam generators A and D, full length

except for rows 1 and 2, which were inspected with the bobbin from tube end to tube

support plate 7 from both hot and cold legs

50 percent, Rows 1 and 2 U-bends, mid-range +Point examination in steam

generators A and D

Mid-range +Point examination of 100 percent of the cold leg peripheral tubes in steam

generators A and D

Dings (free span) > 5 volts: inspect 50 percent of all previously identified and new dings

>5 volts in the hot leg (including the U-bends) with the mid-range +Point probe in steam

generators A and D

Dents (structures) > 2 volts: inspect 50 percent of all previously identified and new dents

>2 volts in the hot leg (including the U-bends) with the mid-range +Point probe in steam

generators A and D

+Point examination of all "I-code" indications that were not resolved after history review

+Point inspection of new wear indications and prior wear indications that have changed

by 10 percent through-wall defect or greater in steam generators A and D

Visual inspection of mechanical and weld plugs

+Point examination of a five percent sample of bobbin indications that have not changed

since the prior inspection (H and S codes)

+Point inspection to bound (all surrounding tubes, at least one pitch removed) the tubes

exhibiting possible loose parts signals during the inspection

+Point inspection of a sample of tubes to support the scale profiling effort

The results, as known to the inspectors at the conclusion of this inspection, are as

follows:

For steam generator A, 6 tubes with wear indication of 40 percent through-wall defect or

greater at one or more anti-vibration bar intersections were plugged. Additionally, one

tube was conservatively plugged for a geometric anomaly. This tube did not exhibit any

cracking characteristic after analysis of the +Point and Ghent probe data.

- 27 -

Enclosure 2

For steam generator D, 10 tubes with wear indication of 40 percent through-wall defect

or greater at one or more anti-vibration bar intersections were plugged. Additionally, one

tube was conservatively plugged for a geometric anomaly. This tube did not exhibit any

cracking characteristic after analysis of the +Point and Ghent probe data.

The inspection procedure specified that, if new degradation mechanisms were identified,

the licensee would verify the analysis fully enveloped the problem of the extended

conditions including operating concerns and that appropriate corrective actions were

taken before plant startup. No new degradation mechanisms were identified by the

eddy current examination results.

The inspection procedure required confirmation that the licensee inspected all areas of

potential degradation, especially areas that were known to represent potential eddy

current test challenges (e.g., top of tube sheet, tube support plates, and U-bends). The

inspectors confirmed that all known areas of potential degradation were included in the

scope of inspection and were being inspected.

The inspection procedure further required verification that repair processes being used

were approved in the technical specifications. At the completion of the inspection, the

inspectors were informed that 18 tubes were to be plugged. The inspectors verified that

the mechanical expansion plugging process used was an NRC-approved repair process.

The inspection procedure also required confirmation of adherence to the technical

specification plugging limit, unless alternate repair criteria had been approved. The

inspection procedure further requires determination whether depth sizing repair criteria

were being applied for indications other than wear or axial primary water stress corrosion

cracking in dented tube support plate intersections. The inspectors determined that the

technical specification plugging limits were being adhered to (i.e., 40 percent maximum

through-wall indication).

If steam generator leakage greater than three gallons per day was identified during

operations or during post shutdown visual inspections of the tube sheet face, the

inspection procedure required verification that the licensee had identified a reasonable

cause based on inspection results and that corrective actions were taken or planned to

address the cause for the leakage. The inspectors did not conduct any assessment

because this condition did not exist.

The inspection procedure required confirmation that the eddy current test probes and

equipment were qualified for the expected types of tube degradation and an assessment

of the site-specific qualification of one or more techniques. The inspectors observed

portions of eddy current tests performed on the tubes in steam generators A and D.

During these examinations, the inspectors verified that: (1) the probes appropriate for

identifying the expected types of indications were being used, (2) probe position location

verification was performed, (3) calibration requirements were adhered to, and (4) probe

travel speed was in accordance with procedural requirements. The inspectors

performed a review of site-specific qualifications of the techniques being used. These

are identified in the attachment.

- 28 -

Enclosure 2

The inspection procedure specified that if loose parts or foreign materials were identified

on the secondary side, the inspectors should review the licensee's evaluation of the

materials and/or complete appropriate repairs of affected steam generator tubes.

Additionally, the licensee should either remove accessible foreign objects or perform an

evaluation of the potential effects of inaccessible object migration and tube fretting

damage. During this inspection, 18 small foreign objects were found in steam

generator A; of these, 7 items were retrieved. There were 34 small foreign objects found

in steam generator D; of these, 18 items were retrieved. These objects, small wires and

sludge rocks, were prioritized and retrieved based on their potential to damage the

steam generator tubes in accordance with Refuel Outage 17 Degradation Assessment

and EPRI 1019039, Steam Generator Management Program: Foreign Object

Prioritization Strategy for Square Pitch Steam Generators. Those items not removed

from the steam generators were evaluated and determined to have no ability to damage

the steam generator tubes during operation. Condition Report AR-00021178 documents

the foreign objects in the licensee's corrective action program. The required chemical

and mechanical effects of these remaining pieces were analyzed with the conclusion of

negligible effects on the respective steam generators. Work Orders 09-321481-000 and

09-321386-000 evaluated the acceptability of the steam generators with these minor

foreign objects remaining.

Finally, the inspection procedure specified review of one-to-five samples of eddy current

test data if questions arose regarding the adequacy of eddy current test data analyses.

The inspectors did not identify any results where eddy current test data analyses

adequacy was questionable.

These actions constitute completion of the requirements for Section 02.04 of Inspection

Procedure IP 71111.08.

b.

Findings

No findings of significance were identified.

.5

Identification and Resolution of Problems (71111.08-02.05)

a.

Inspection Scope

The inspection procedure required review of a sample of problems associated with

inservice inspections documented by the licensee in the corrective action program for

appropriateness of the corrective actions.

The inspectors reviewed nine condition reports which dealt with inservice inspection

activities and found the corrective actions were appropriate. The specific condition

reports reviewed are listed in the documents reviewed section. From this review, the

inspectors concluded that the licensee has an appropriate threshold for entering issues

into the corrective action program and has procedures that direct a root cause evaluation

when necessary. The licensee also has an effective program for applying industry

- 29 -

Enclosure 2

operating experience. Specific documents reviewed during this inspection are listed in

the attachment.

These actions constitute completion of the requirements for Section 02.05 of Inspection

Procedure IP 71111.08.

b.

Findings:

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a.

Inspection Scope

There were no opportunities to inspect operator requalification in the fourth quarter.

There were zero activities completed for quarterly licensed-operator requalification as

defined in Inspection Procedure IP 71111.11.

b.

Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

October 27, 2009, 125Vdc nonsafety-related PK system

December 17, 2009, Component cooling water system

December 18, 2009, Source range neutron monitors

October 6, 2009, Residual heat removal system

December 21, 2009, Offsite power supplies

December 22, 2009, Intermediate range neutron monitors

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

Implementing appropriate work practices

Identifying and addressing common cause failures

Scoping of systems in accordance with 10 CFR 50.65(b)

- 30 -

Enclosure 2

Characterizing system reliability issues for performance

Charging unavailability for performance

Trending key parameters for condition monitoring

Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)

Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of six quarterly maintenance effectiveness

samples as defined in Inspection Procedure IP 71111.12-05.

b.

Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

November 20, 2009, Emergent work on control room door ventilation boundary

October 15, 2009, Corrosion on containment cooler A

October 13, 2009, Emergent work on annunciator power supply failures

October 10 to November 17, 2009, Shutdown risk assessments

November 18, 2009, Technical Specification 3.0.4.b risk assessment for Mode 4

to Mode 3

November 23, 2009, Emergent work for oil loss from centrifugal charging pump A

- 31 -

Enclosure 2

The inspectors selected these activities based on potential risk significance relative to

the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three maintenance risk assessments and

emergent work control inspection sample as defined by Inspection

Procedure IP 71111.13-05.

b.

Findings

.1

Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65(a)(4)

involving the failure to adequately perform shutdown risk assessments during Refueling

Outage 17.

Description. While reviewing daily risk assessments during Refueling Outage 17, the

inspectors noted discrepancies in the calculation of the risk conditions of the shutdown

safety function condition. As a result, the inspectors reviewed the AP 22B-001, Outage

Risk Assessment, and Form APF 22B-001-02, Daily Shutdown Risk Assessment.

Wolf Creek uses Procedure AP 22B-001, to implement the requirements of 10

CFR 50.65(a)(4) during shutdown conditions (Modes 4, 5, 6, and defueled). In the

references section, the procedure lists NUMARC 93-01, Section 11, Assessment of

Risk Resulting from Performance of Activities, as well as Regulatory Guide 1.182 in

which the NRC endorses NUMARC 93-01, Section 11, dated February 2000. Wolf

Creek has no NRC approved exceptions to Regulatory Guide 1.182. NUMARC 93-01,

Section 11.3.5, provides a scope of five key Shutdown Safety Functions: decay heat

removal capability, inventory control, electric power availability, reactivity control, and

containment. Sections 11.3.6.1 through 11.3.6.5 provide specifics for each shutdown

function. Overall, the inspectors found several examples in which the five aspects

NUMARC 93-01, Section 11, were not correctly implemented for risk assessments.

Form APF 22B-001-02 defines Condition 3 or High Risk as only one safety train is

available to satisfy the shutdown safety function. In the examples below, this

contradicted with Wolf Creeks actions.

For the Decay Heat Removal Shutdown Safety Function, Procedure APF 22B-001-02

did not direct consideration of containment closure time per NUMARC 93-01,

Section 11.3.6.1. The inspectors cross-referenced the daily shutdown risk assessment

forms with the equipment out-of-service list maintained in the control room log and found

three such instances of this occurring. First, on October 16 and 17, 2009, during the

- 32 -

Enclosure 2

core offload, the reactor building equipment hatch was listed as closed during fuel

movement; however, the equipment out-of-service list showed the equipment hatch as

open from October 10 through November 15, 2009. Secondly, from October 14-17,

2009, and again on November 5-11, 2009, the reactor building auxiliary access hatch

was on the equipment out-of-service list because the interlocks were defeated to install

a temporary closure device. The daily risk assessment did not analyze this condition

which had the potential to impact the outcome of the risk assessment. The third

instance occurred on November 16, 2009, when the reactor building personnel hatch

failed to meet the surveillance requirement acceptance criteria. This was also not

analyzed for its effect on containment closure.

For the (Electric) Power Availability Shutdown Safety Function,

Procedure APF 22B-001-02 did not explicitly direct consideration of ac and dc

instrumentation and control power availability per NUMARC 93-01, Section 11.3.6.3.

The inspectors cross-referenced the daily shutdown risk assessment forms with the

equipment out-of-service list maintained in the control room log archive and found two

such instances of this occurring. First from October 19 through 25, 2009, the 125Vdc

60-Cell Battery 4 was inoperable pending further analysis due to positive plate material

separation identified during a visual inspection. The corresponding NK04 electrical bus

was incorrectly considered available on the six daily risk assessments performed during

that time period. The second instance occurred on November 6 through 10, 2009, when

the 125Vdc 60-Cell Battery 3 inoperable pending further analysis due to several cell

abnormalities identified during a visual inspection. The corresponding NK03 electrical

bus was incorrectly considered available on the five daily risk assessments performed

during that time period. Furthermore, these dc power unavailabilities were listed on the

risk assessment, but were not factored into its outcome (or color).

For the Containment Shutdown Safety Function, Procedure APF 22B-001-02 did not

direct consideration of the availability of ventilation and radiation monitoring equipment

with respect to the filtration and monitoring of releases per NUMARC 93-01,

Section 11.3.6.5. The inspectors again cross-referenced the daily shutdown risk

assessment forms with the equipment out-of-service list maintained in the control room

log and identified two such instances of this occurring. The first instance occurred

during core offload on October 17, 2009. At that time, the availability of Containment

Atmospheric Radiation Monitor GTRE0031 was degraded because it was being powered

by temporary power. The normal source, safety bus NB02, was de-energized for

maintenance from October 17 through 25, 2009. The second instance occurred during

core reload on November 5 and 6, 2009, when the GTRE0021B was removed from

service from October 29 through November 28, 2009, per the equipment out-of-service

list. Neither of these components was listed in the daily risk assessment, nor was their

impact quantified in the determination of the risk level (or color).

For the Decay Heat Removal Shutdown Safety Function, only residual heat removal

and steam generators can actually perform the function of heat removal. The risk

assessments credited reactor cavity level greater than 23 feet above the vessel flange

and a greater than 4-hour time to boil in the decay heat removal function. Thus, this

configuration would be a permissible, moderate risk condition even if there were no

active means of removing heat from the reactor. The inspectors cross-referenced the

- 33 -

Enclosure 2

daily shutdown risk assessment forms with the equipment out-of-service list and

identified two instances of this occurring. First, on October 10, 2009 at 10:29 a.m., and

again on November 13 through 17, 2009, the risk assessments specified that steam

generators were available for heat removal when the auxiliary feedwater system was

unavailable because its safety-related water source (essential service water) was

isolated by Clearance Order C17-R-OP-S-005. Steam generators were available for

reflux cooling. Wolf Creek credits reflux cooling using EPRI Technical Report 102972,

Reflux Cooling: Application to Decay Heat Removal During Shutdown Operations.

The earliest EPRI analyzed scenario is 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after shutdown; however, on

October 10, 2009, only 10.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> following shutdown, the decay heat load would be

significantly higher and warrant further analysis. The inspectors concluded that since

this condition was unanalyzed, it could not be credited and a steam generator feedwater

source would be required for such a short time after reactor shutdown. The decay heat

removal Shutdown Safety Function was categorized as normal risk (green) when it

should have been moderate risk (yellow) for the two risk assessments performed on

October 10, 2009. The other risk assessments that use reflux cooling were bounded by

the EPRI analysis. Lastly, the inspectors reviewed spent fuel pool cooling on

October 30, 2009. The risk assessment form specified one train was available and

resulted in moderate risk (yellow); however, red risk was defined as one safety train

available for the function. Although not an input to the color, the form specified normal

and alternate makeup water sources to the spent fuel pool. Inspectors interviewed

senior operators to identify the normal and alternate sources. One indicated that the

refueling water storage tank through the spent fuel pool transfer pumps was the normal

source. Another indicated demineralized water was the makeup source. For the

alternate makeup source, one indicated essential service water while another stated it

was fire water. In any case, none of the sources were specified and tracked by the risk

assessment form to mitigate the loss of one fuel pool cooling train.

For the [Electric] Power Availability Shutdown Safety Function, a loss of offsite power,

or loss of both diesel generators, combined with no switchyard activities is categorized

as a low risk condition. Furthermore, a station blackout with no switchyard activities in

progress is a moderate risk condition. Inspectors found that this resulted in an

inadequate risk assessment for electrical power in that the risk assessment would permit

shutdown activities without any available sources of ac power. Wolf Creek categorized

one in-service power source as moderate risk (yellow) rather than high risk. This was in

contrast to the definition of high risk in which only one safety train available to satisfy the

function. The inspectors cross-referenced the daily shutdown risk assessment forms

with the equipment out-of-service list maintained in the control room log and found that

on November 8, 2009, at 8:57 a.m. the risk assessment listed two diesel generators as

being available; however, the equipment out-of-service list indicated that emergency

diesel generator A was out of service because essential service water train A was

unavailable from November 5, 2009, at 4:37 a.m. until November 8, 2009, at 1:30 p.m.

When the credit for emergency diesel generator A is removed, the risk assessment

outcome changes from normal risk (green) to moderate risk (yellow). The second

instance occurred for the daily risk assessment performed between October 31 and

November 4, 2009, which lists two diesel generators as being available. However, the

equipment out-of-service list indicated that emergency diesel generator B was out of

- 34 -

Enclosure 2

service because essential service water Train B was unavailable from October 16, 2009,

at 10:05 p.m. until November 5, 2009, at 4:19 a.m. On all five daily risk assessments

performed between October 31 and November 4, 2009, if the credit for the second diesel

generator were removed, the outcome of the risk assessment changed from normal risk

to moderate risk.

Analysis. The failure to meet shutdown risk assessment requirements in the shutdown

risk assessment process is a performance deficiency. Traditional enforcement does not

apply since there were no actual safety consequences or potential for impacting the

NRC's regulatory function, and the finding was not the result of any willful violation of

NRC requirements or Wolf Creek procedures. The inspectors determined that this

finding impacted the Mitigating Systems Cornerstone and was more than minor because

it involved incorrect risk assessments that changed the outcome or color of the

assessments. Per Inspection Manual Chapter 0609, Appendix K, Maintenance Risk

Assessment and Risk Management Significance Determination Process, licensees who

only perform qualitative analyses of plant configuration risk due to maintenance

activities, the significance of the deficiencies must be determined by an internal NRC

management review using risk insights where possible in accordance with Inspection

Manual Chapter 612, Power Reactor Inspection Reports. The NRC management

review concluded that this finding was of Green safety significance because missing risk

management actions did not result in loss of key shutdown risk functions. Additionally,

the cause of the finding has a human performance crosscutting aspect in the area

associated with the resources. Specifically, Wolf Creek did not ensure that

Procedure APF 22B-001-02 was complete, accurate, and up-to-date H.2(c).

Enforcement. Title 10 CFR 50.65(a)(4) states, in part, that before performing

maintenance activities (including but not limited to surveillance, postmaintenance testing,

and corrective and preventive maintenance), the licensee shall assess and manage the

increase in risk that may result from the proposed maintenance activities. Contrary to

the above, between October 10, and November 17, 2009, Wolf Creek did not

appropriately assess and manage the increase in risk resulting from proposed

maintenance activities. Specifically, Form APF 22B-001-02 did not appropriately

consider electrical power, decay heat removal, and containment when assessing

shutdown risk. Because the finding is of very low safety significance and has been

entered into the corrective action program as condition reports 22295 and 22296, this

violation is being treated as a noncited violation, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000482/2009005-04, Failure to Incorporate Requirements

of Regulatory Guide 1.182 into Daily Shutdown Risk Assessments.

.2

Introduction. On November 18, 2009, the inspectors identified a Green noncited

violation of Technical Specification 3.0.4.b for ascension from Mode 4 to Mode 3 without

establishing required risk management actions.

Description. On the morning of November 18, 2009, the turbine-driven auxiliary

feedwater pump was inoperable per technical specification 3.0.4.b as specified in the

control room log at 11:53 p.m. the previous day upon ascension from Mode 4 into

Mode 3 at 12:24 a.m. Technical specification 3.0.4.b permits mode ascension after

performance of a risk assessment to address the inoperable components and

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Enclosure 2

consideration and implementation of risk management actions to maintain safety in the

next mode. This condition is permissible for auxiliary feedwater per Technical

Specification LCO 3.7.5 so long as the ascension is below Mode 1. The entry was made

using an operational risk assessment Form APF 22C-003-01 in accordance with

Technical Specification LCO 3.0.4.b. The risk assessment on November 17, 2009,

specified:

1.

The turbine-driven auxiliary feedwater pump restoration following Surveillance

Requirement 3.7.5.2, completion is expected within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> of entering Mode 3.

2.

As a compensatory measure [risk management action], protected train signs

would be placed on the doors to the motor-driven auxiliary feedwater pumps A

and B room doors.

A walkdown conducted by the inspector at 10:30 a.m. on November 18, 2009, found that

the protected train signs on the motor-driven auxiliary feedwater pump rooms specified

by the operational risk assessment were not in place. Also, a maintenance crew was

performing radiography in the motor-driven auxiliary feedwater pump Room B. A further

review of the control room logs revealed that motor-driven auxiliary feedwater pump

comprehensive pump testing, flow path verification, and containment isolation valve

verification testing were scheduled and performed, making both motor-driven auxiliary

feedwater pumps A and B inoperable (at separate times) during the morning of

November 18, 2009, while turbine-driven auxiliary feedwater was still inoperable.

Operators did make proper entry into Technical Specification 3.7.5, Condition C, for two

of three auxiliary feedwater trains inoperable; however, this configuration was not

analyzed in the risk assessment. Immediately following the walkdown, the inspector

discussed the issue with the shift manager, the protected train signs were installed on

the motor-driven auxiliary feedwater pump room doors and a condition report was

initiated. Wolf Creek determined that an informal mode ascension check off list was

used that conflicted with the risk assessment performed for Technical

Specification 3.0.4.b.

Analysis. Mode ascension under Technical Specification LCO 3.0.4.b without

establishing required risk management actions is a performance deficiency. Traditional

enforcement does not apply since there were no actual safety consequences or potential

for impacting the NRC's regulatory function, and the finding was not the result of any

willful violation of NRC requirements or Wolf Creek procedures. The inspectors

determined that the violation was more than minor because it was associated with the

configuration control and alignment attribute of the Mitigating Systems Cornerstone and

affected the cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences. The

configuration control issues not only included the work being completed on the

turbine-driven auxiliary feedwater pump, but also included containment isolation valve

testing and radiography that was performed on the motor-driven auxiliary feedwater

pumps which was not included in the risk assessment. The inspector used Inspection

Manual Chapter 0609.04, Phase 1 SDP - Worksheet, to determine that the finding was

of very low safety significance (Green) because it did not result in a loss of system safety

function; exceed allowable technical specification outage time; and was not a seismic,

- 36 -

Enclosure 2

flooding, or severe weather concern. Additionally, the cause of the finding has a human

performance crosscutting aspect in the area associated with the decision making.

Specifically, Wolf Creek used a risk assessment form and informal mode change form to

communicate between departments the requirement for risk management actions. The

two forms were in conflict, and the personnel who implemented the risk management

actions were not informed H.1(c).

Enforcement. Wolf Creek Technical Specification LCO 3.0.4.b states, in part, When an

LCO is not met, entry into a MODE or other specified condition in the Applicability shall

only be made after performance of a risk assessment addressing inoperable systems

and components, consideration of the results, determination of the acceptability of

entering the MODE or other specified condition in the Applicability, and establishment of

risk management actions, if appropriate. Prior to MODE ascension with the

turbine-driven auxiliary feedwater pump inoperable, Wolf Creek performed a risk

assessment and identified risk management actions. Contrary to the above, on

November 18, 2009, at 12:24 a.m. Wolf Creek invoked Technical Specification 3.0.4.b to

ascend from Mode 4 to Mode 3 without implementing the risk management actions

required by the risk assessment performed to justify the Mode change with the

turbine-driven auxiliary feedwater pump inoperable. Because the finding is of very low

safety significance and has been entered into the corrective action program as Condition

Report 00021926, this violation is being treated as a noncited violation, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-05, Mode

Change under Technical Specification 3.0.4.b Without Required Risk Management

Actions.

.3

Introduction. On October 15, 2009, the inspectors identified a violation of 10 CFR

Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for failure to

follow Procedure AP 28A-100, Condition Reports. Wolf Creek failed to initiate a

condition report for evaluation of corrosion on containment cooler A piping.

Description. On October 15, 2009, the inspectors identified dried white and brown

deposits on vertical piping from insulation seams on containment cooler A. The

inspectors identified the condition to Wolf Creek. On October 17, Wolf Creek completed

Work Order 09-321113-000 to remove the insulation and found significant corrosion of

piping and flanges for containment cooler A. Work Order 09-321113-000 stated that the

cause of the corrosion was unknown. Wolf Creek informed the inspectors that the cause

of the corrosion was condensation. The inspectors noted that since no ultrasonic testing

had been performed, leakage from through-wall defects could not be eliminated as a

cause. Wolf Creek later informed the inspectors that the visual inspection showed no

through wall defects. The inspectors again challenged Wolf Creek since no ultrasonic

testing was performed to demonstrate that through wall defects could be eliminated as a

cause. The inspectors reviewed Procedure AP 28A-100, Condition Reports,

Revision 10, Attachment C. Attachment C required condition reports when equipment

issues require evaluation beyond the work controls (work order) process.

Procedure AP 28A-100 defines an adverse condition as one that could impact nuclear

safety. Wolf Creek subsequently initiated Condition Report 20964 on October 21, 2009,

stating that there was extensive corrosion on containment cooler A and that all

containment coolers could be affected. Condition Report 20964 went on to evaluate the

- 37 -

Enclosure 2

piping insulation and how it did not prevent condensation on the piping which allowed

the corrosion.

On October 23 and October 26, Wolf Creek initiated several work requests to perform

ultrasonic testing of containment coolers A, B, and C. Wolf Creek initiated the work

order to perform piping and flange thickness measurements which were found to be

satisfactory. Wolf Creek engineering determined that containment coolers A, B, and C

had piping flange studs that needed to be replaced due to corrosion. From November 1

to November 2, a total of 32 studs and 96 nuts were replaced for the three coolers. On

November 8 and 11, 2009, Wolf Creek completed engineering dispositions to address

the cause and the results of the ultrasonic testing. Condition Report 22443 also

identified the need for more ultrasonic inspections in the next refueling outage to verify

acceptable corrosion rates. On December 16, 2009, Wolf Creek initiated Condition

Report 22443 which described the lack of a timely condition report to determine a cause

of the corrosion.

Analysis. The inspectors determined that the failure to follow Procedure AP 28A-100,

Appendix C, was a performance deficiency. Traditional enforcement does not apply

since there were no actual safety consequences or potential for impacting the NRCs

regulatory function, and the finding was not the result of any willful violation of NRC

requirements or Wolf Creek procedures. This issue was more than minor because it

was associated with the equipment performance attribute of the Mitigating Systems

Cornerstone and affected the cornerstone objective to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609.04, the issue screened to Green

because there was not a loss of operability and the finding did not screen as potentially

risk significant due to a seismic, flooding, or severe weather initiating event. A

crosscutting aspect was identified in the problem identification and resolution area of the

corrective action program. Specifically, Wolf Creek failed to implement a corrective

action program with a low threshold for identifying issues P.1.a].

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality be described by

documented instructions, procedures or drawings appropriate to the circumstances and

be accomplished in accordance with these instructions, procedures or drawings.

Procedure AP 28A-100, Attachment C, Equipment Problems Requiring a Condition

Report, requires, in part, that condition reports be written where further evaluation is

needed outside the work control process. Contrary to the above, from October 15 to 23,

2009, Wolf Creek failed to complete an activity affecting quality in accordance with

documented procedures appropriate to the circumstances. Specifically, Wolf Creek

failed to write a condition report for corrosion on containment cooler A after Work

Order 09-321113-000 stated that the cause of the corrosion was unknown. Because this

violation was determined to be of very low safety significance and was placed in the

corrective action program as Condition Reports 20964 and 22443, this violation is being

treated as a noncited violation in accordance with Section VI.A.1 of the Enforcement

Policy: NCV 05000482/2009005-06, Failure to Follow Corrective Action Procedure.

- 38 -

Enclosure 2

.4

Introduction. On November 23, 2009, a self-revealing violation of Technical

Specification 5.4.1.a was reviewed by the inspectors after a technician failed to follow

procedures and emptied 45 gallons of oil from centrifugal charging pump A.

Description. On November, 23, 2009, a technician loosened the wrong nut and removed

the thermowell for Temperature Indicator BG TI-0036 on centrifugal charging pump A. At

the time, the auxiliary lube oil pump was running. The auxiliary lube oil pump normally

runs while the pump is in standby. This emptied 45 gallons of oil from the pump.

Removal of the temperature indicator normally would not affect operability since the oil

temperature indication is not required; however, the pump cannot function without lube

oil. Control room operators declared the pump inoperable and entered Technical

Specification 3.5.2. Approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> later, the thermowell and oil were replaced,

the pump was leak tested and Technical Specification 3.5.2, Condition A was exited.

Wolf Creek performed a root cause analysis for this issue under Condition

Report 21993. During interviews, the technician stated that he performed a 2 minute

self-check (a recognized error reduction technique at Wolf Creek) but failed to identify

the correct nut to loosen. This task is a required training task for these temperature

indicators, which involves a similar training rig. The technician stated that he understood

the difference between the thermowell nut and the temperature indicator but failed to

make the differentiation on November 23. The technician and the supervisor discussed

the work, but the communication was inadequate because the technician was left with

the idea to perform the work independently, and the supervisor believed that the

technician was only going to perform a walkdown of the indicator. The prejob briefing

standard at Wolf Creek required supervisor approval for a self-briefing.

Analysis. The failure to follow Procedure STN IC-294A and correctly remove the

detector was considered a performance deficiency. Traditional enforcement does not

apply since there were no actual safety consequences or potential for impacting the

NRC's regulatory function, and the finding was not the result of any willful violation of

NRC requirements or Wolf Creek procedures. The finding was more than minor

because it was associated with the equipment performance attribute of the Mitigating

Systems Cornerstone, and it affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. The inspectors evaluated the significance of this finding

using Phase 1 of Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, and determined that the finding was of very low safety

significance (Green) because the pump was inoperable for less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Also, the

finding did not screen as potentially risk significant due to a seismic, flooding, or severe

weather initiating event. The inspectors identified a human performance crosscutting in

the area of work practices because a 2-minute self-check and communication with the

supervisor failed to prevent the event H.4.a].

Enforcement. Technical Specification 5.4.1.a requires the implementation of written

procedures described in Regulatory Guide 1.33, Revision 2, Appendix A. Section 9.A of

Regulatory Guide 1.33 requires procedures for performing maintenance that can affect

the performance of safety-related equipment. Procedure STN IC-294A, Calibration of

CCP A Outboard Bearing and Lube Oil Supply Temperature Indicators BGTI0036

- 39 -

Enclosure 2

and BGTI0040, Revision 0, step 8.2.1, requires that the temperature detector be

removed from its thermowell for calibration. Contrary to the above, on November 23,

2009, a worker removed the thermowell and breached the lube oil subsystem. Because

this violation was determined to be of very low safety significance and was placed in the

corrective action program as Condition Report 21993, this violation is being treated as a

noncited violation in accordance with Section VI.A.1 of the Enforcement Policy:

NCV 05000482/2009005-07, Failure to Follow Procedure Results in Draining of

Emergency Core Cooling System Pump Oil.

1R15 Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed the following issues:

October 9, 2009, Source range nuclear instrument (NI)-31 response

November 5, 2009, Essential service water pump seismic operability

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and USAR to

the licensees evaluations, to determine whether the components or systems were

operable. Where compensatory measures were required to maintain operability, the

inspectors determined whether the measures in place would function as intended and

were properly controlled. The inspectors determined, where appropriate, compliance

with bounding limitations associated with the evaluations. Additionally, the inspectors

also reviewed a sampling of corrective action documents to verify that the licensee was

identifying and correcting any deficiencies associated with operability evaluations.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three operability evaluations inspection samples

as defined in Inspection Procedure IP 71111.15-05

b.

Findings

.1

Introduction. On November 5, 2009, the inspectors identified a Green noncited violation

of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

for failure to perform an adequate operability evaluation as required by procedure.

Description. On November 1, 2009, Wolf Creek was defueled for Refueling Outage 17,

and essential service water pump A was being replaced. On November 1, 2009, Wolf

Creek found that the as-constructed clearances at the essential service water pump A

flange did not meet design requirements. This allowed the pump column to flex up to

0.125 inches until it would engage the seismic supports. The pumps were designed to

be rigidly restrained. This resulted in Condition Reports 21400 and 21572. Wolf Creek

- 40 -

Enclosure 2

completed Operability Evaluation EF-09-010 that provided the basis for the past

operability of essential service water Pump A and future operability of essential service

water pump B on November 1, 2009, and initiated Condition Report 22400 to correct the

clearances.

On November 5, 2009, the inspectors reviewed Operability Evaluation EF-09-010. The

evaluation concluded that the increased movement of the pump would increase stresses

to 10 ksi, which was below the specified allowable ASME Code Section III limit of

17.5 ksi. The evaluation identified requirements that the pumps shall operate during and

after a safe shutdown earthquake as one of the design basis functions as required per

10 CFR Part 50, Appendix A, General Design Criterion 2. These seismic design

requirements are contained in Sections 3.9(B) and 9.2.1 of the USAR. The inspectors

found that the operability evaluations technical basis was inadequate due to the

following: (1) the evaluation did not contain a formal calculation that demonstrated that

stresses were below limits, (2) the evaluation only considered operating basis

earthquake accelerations and not the larger safe shutdown earthquake accelerations,

(3) the evaluation did not contain a calculation to demonstrate that the pump impeller

clearances were allowable if an earthquake occurred while the pump was running, and

(4) the method of analysis for the stresses was not described as an appropriate

alternative method to the original stress calculation done with the SAP V computer

program. The inspectors could not verify that the simplified method was appropriate.

The inspectors reviewed Procedure AP 26C-004, Technical Specification Operability,

Revision 20 and Procedure AP 28-001, Operability Evaluations, Revision 17.

Procedure AP 26C-004, step 6.2.6, states that documentation for prompt operability

evaluations shall include information needed to support operability. Step 4.5 states that

safety functions specified in the current licensing basis shall be met.

Procedure AP 28-001, Operability Evaluations, step 4.9, also describes that the

specified safety functions in the current licensing basis shall be met. Step 6.1.7 states

that design basis events and safety evaluations should be considered. There is no

description of the use of alternative analysis methods in AP 28-001 or AP 26C-004 that

is consistent with Regulatory Information Summary 2005-20, Section C.4.

On November 7, 2009, Wolf Creek initiated Condition Report 21572 to resolve the items

identified above. Wolf Creek completed Operability Evaluation EF-09-010, Revision 1,

on December 14, 2009. The inspectors reviewed Revision 1 and determined the above

identified deficiencies still existed. Wolf Creek performed a third revision to Operability

Evaluation EF-09-010 and initiated Condition Report 22798. The four items were

resolved with Operability Evaluation EF-09-010, Revision 2 which contained drawings

and calculations to demonstrate that the pumps were seismically qualified and that the

simplified calculations were appropriate. In Revision 2, the calculated stresses

increased to 16.4 ksi but were still below the limit of 17.5 ksi.

Analysis. The failure to perform an adequate operability evaluation per

Procedures AP 28-001 and AP 26C-004, was a performance deficiency. Traditional

enforcement does not apply since there were no actual safety consequences or potential

for impacting the NRC's regulatory function, and the finding was not the result of any

willful violation of NRC requirements or Wolf Creek procedures. The inspectors

- 41 -

Enclosure 2

determined that this finding was more than minor because it is associated with the

equipment performance attribute for the Mitigating Systems Cornerstone, and it affected

the cornerstone objective to ensure the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core

damage). Specifically, this issue relates to the availability and reliability examples of the

equipment performance attribute because a latent common mode failure mechanism

was not correctly evaluated. The inspectors evaluated the significance of this finding

using Phase 1 of Inspection Manual Chapter 0609, Appendix A, "Significance

Determination of Reactor Inspection Findings for At Power Situations," and determined

that the finding was of very low safety significance (Green) because the issue was not a

design or qualification deficiency confirmed to result in loss of operability or functionality,

did not represent a loss of system safety function, an actual loss of safety function of a

single train for greater than its technical specification allowed outage time, an actual loss

of safety function of a nontechnical specification risk-significant equipment train, and did

not screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. The cause of the finding has a problem identification and resolution

crosscutting aspect in the area associated with the corrective action program because

Wolf Creek failed to thoroughly evaluate the failure mechanism such that the resolutions

address the causes and extent of conditions, as necessary P.1.c].

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions or procedures of a type appropriate to the circumstances,

accomplished in accordance with those instructions or procedures, and contain

acceptance criteria to demonstrate that the activity was successfully accomplished.

Procedure AP 26C-004, Technical Specification Operability, Revision 20, implements

this requirement and states, in part, that continued operability decisions shall be made in

accordance with Procedure AP 28-001, Operability Evaluations, Revision 17.

Procedure AP 28-001 requires, in part, that operability evaluations shall demonstrate

that equipment meets its design functions. Per Sections 3.9(B) and 9.2.1 of the USAR,

the essential service water pumps are designed to withstand a safe shutdown

earthquake. Contrary to the above, from November 1, 2009, to January 13, 2010,

Operability Evaluation EF-09-010, Revisions 0 and 1, did not demonstrate that the

essential service water pumps could withstand a safe shutdown earthquake.

Specifically, no calculations existed to demonstrate allowable stresses and pump

impeller clearances. Because the finding is of very low safety significance and has been

entered into the corrective action program as Condition Reports 22798 and 21572, this

violation is being treated as a noncited violation, consistent with Section VI.A of the

NRC Enforcement Policy: NCV 05000482/2009005-08, Inadequate Operability

Evaluation of Essential Service Water Pumps.

.2

Introduction. The inspectors identified a Green, noncited violation of Technical

Specification 3.3.1, Condition I, for making positive reactivity addition prohibited by

technical specifications in Mode 2 because one source range nuclear instrument

channel was inoperable.

Description. On August 19, 2009, at 3:47 p.m., a loss of offsite power and reactor trip

occurred. As a result, cavity cooling fans were lost causing an increase in air

- 42 -

Enclosure 2

temperature in the reactor cavity. Shortly thereafter, the indicated count rate on source

range nuclear instrument NI-31 began increasing from the expected value of about 250

counts per minute (cpm) to 15,000 cpm and then to a maximum of 27,000 cpm over an

8-hour period. Control room operators declared the source range channel NI-31

inoperable as a result of this abnormal behavior. Power to the cavity fans was restored

around 1 a.m. on August 20, 2009, and the source range nuclear instrument NI-31 count

rate returned to its expected value below 250 cpm, based on its anticipated reading

relative to source range NI-32 which did not experience any increase in count rate with a

loss of cavity cooling.

Wolf Creek concluded, based on feedback from the vendor, the most likely cause of the

abnormal readings was moisture intrusion at the cable to detector connection at the

base of the detector inside the reactor cavity. As long as cavity cooling remained

available, the moisture intrusion would not be an issue. Based on this information, Wolf

Creek declared the source range NI-31 operable restarted from the forced outage on

August 23, 2009. Wolf Creeks operability evaluation failed to identify that safety-related

equipment was now reliant on nonsafety cavity cooling fans and nonsafety electrical

power to those fans. The source range instruments NI-31 and -32 are required to be

operable in Mode 2 below the P-6 interlock to monitor the approach to criticality.

During this time, the resident inspectors questioned the operability of source range

instrument NI-31. When entering Refueling Outage 17, a power supply failure in the

control cabinet caused source range NI-31 to fail upon demand during shutdown. On

October 7, 2009, Wolf Creek performed another operability evaluation that stated that

the source range was operable because it had passed its surveillance tests during the

last refueling outage that ended in May 2008. The inspectors noted that this evaluation

did not address the observed problem and therefore did not provide a reasonable basis

for operability. On October 28, 2009, during interviews with Wolf Creek engineering

personnel, the inspectors learned that the original operability determination used to

restart from the forced outage was inaccurate because the equipment configuration in

the field was different than described in the operability determination. The detectors are

in fact hard wired and there are no cabling connections until the containment bio-shield

wall, therefore, no connectors would be affected by the reactor cavity temperature

increase following the loss of cavity cooling fans. Consequently, there was no valid

explanation for the increase in count rate observed on August 19, 2009. Shortly

thereafter, Wolf Creek replaced the source range NI-31 detector before restart from

Refueling Outage 17 to definitively restore operability to the channel.

On November 13, 2009, the resident inspectors observed the removal of source range

Detector SE-0031 from the reactor cavity. There was some minor damage to the outer

layer of cable wrap, however, nothing was observed that could conclusively explain the

detectors malfunction on August 19, 2009, or ensure its future operability. Wolf Creek

USAR, Chapter 15, credits low power reactor trips as being terminated by the power

range instruments. The power range instruments are not required to be operable in

Mode 3. USAR, Chapter 15, credits the source range and intermediate range reactor

trips to stop reactivity excursions at a much lower power. This allows technical

specifications to credit these trips in Mode 3. During the shutdown in August 2009, rod

drive motor-generator set testing was performed which cycled the reactor trip breakers

- 43 -

Enclosure 2

and made the control rods capable of withdrawal. The inspectors also reviewed the

technical specification bases for the source range which stated that they are required to

perform a monitoring function of neutron levels and provide indication of reactivity

changes that may occur.

Analysis. Reactivity addition with source range channel nuclear instrument-31

inoperable is a performance deficiency. The finding was more than minor because it

was associated with the configuration control (reactivity control) attribute of the Barrier

Integrity Cornerstone, and it affected the cornerstone objective to provide reasonable

assurance that physical design barriers (fuel cladding, reactor coolant system, and

containment) protect the public from radionuclide releases caused by accidents or

events. The inspectors evaluated the significance of this finding using Phase 1 of

Inspection Manual Chapter 0609.04, and determined that the finding screened to Green

because the finding only affected the fuel barrier. Additionally, the cause of the finding

has a human performance crosscutting aspect in the area associated with the decision

making. Specifically, Wolf Creek did not use conservative assumptions in decision

making and adopt requirements to demonstrate that the proposed action is safe in order

to proceed rather than a requirement to demonstrate that it is unsafe in order to

disapprove the action, when performing an operability evaluation for the source range

Nuclear Instrument 31 detector prior to restarting from a forced outage H.1(b).

Enforcement. Wolf Creek Technical Specification LCO 3.3.1 Reactor Trip System

Instrumentation, Condition I, requires immediate suspension of all operations activities

involving positive reactivity additions when one source range channel is inoperable while

in Mode 2. Contrary to the above on August 22, 2009, at 11:10 a.m., Wolf Creek

entered Mode 2 with one source range channel inoperable and continued withdrawing

control rods until the reactor was critical at 11:54 a.m. At that time, Wolf Creek went

above the P-6 interlock and source range monitoring was no longer required by technical

specifications. Because the finding is of very low safety significance and has been

entered into the corrective action program as Condition Report 20208, this violation is

being treated as a noncited violation, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000482/2009005-09, Positive Reactivity Addition

Prohibited by technical specifications while in Mode 2.

1R18 Plant Modifications (71111.18)

Permanent Modifications

The inspectors reviewed key affected parameters associated with energy needs,

materials, replacement components, timing, heat removal, control signals, equipment

protection from hazards, operations, flow paths, pressure boundary, ventilation

boundary, structural, process medium properties, licensing basis, and failure modes for

the permanent modifications listed below.

December 16, 2009, Instrument setpoints for reactor coolant pump thermal

barrier isolation and Valve EGHV62

- 44 -

Enclosure 2

The inspectors reviewed key parameters associated with energy needs, materials,

replacement components, timing, heat removal, control signals, equipment protection

from hazards, operations, flow paths, pressure boundary, ventilation boundary,

structural, process medium properties, licensing basis, and failure modes for the

permanent modification identified as configuration Change Package 013096.

The inspectors verified that modification preparation, staging, and implementation did not

impair emergency/abnormal operating procedure actions, key safety functions, or

operator response to loss of key safety functions; postmodification testing will maintain

the plant in a safe configuration during testing by verifying that unintended system

interactions will not occur; systems, structures and components, performance

characteristics still meet the design basis; the modification design assumptions were

appropriate; the modification test acceptance criteria will be met; and licensee personnel

identified and implemented appropriate corrective actions associated with permanent

plant modifications. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of one sample for permanent plant modifications

as defined in Inspection Procedure IP 71111.18-05.

b.

Findings

Introduction. On December 16, 2009, inspectors identified a Green noncited violation of

10 CFR Part 50, Appendix B, Criterion III, Design Control, involving failure to obtain

vendor design data for a modification.

Description. On December 16, 2009, the inspectors reviewed configuration change

Package 013096 from August 2009 which modified the upper flow limit through the

reactor coolant pump thermal barrier heat exchangers from 60 to 68 gpm. The change

package cited an internal memo from 1992 as the justification for the increased flow.

The inspectors reviewed the internal memo and noted that it described the thermal

barrier outlet valves going closed on high flow. It also indirectly described a telephone

conversation with a Westinghouse representative who stated that the thermal barriers

were capable of up to 90 gpm sustained flow. The inspectors found no accompanying

data from Westinghouse to justify this claim. Procedure AP 05-005, Design Control,

required that vendor data be obtained in accordance with Procedure AP 05-013, Review

of Vendor Technical Documents, Revision 7A. The inspectors reviewed

Procedure AP 05-013 and noted that it stated that documentation would be obtained

from the vendor consistent with procurement standards for acceptance.

Procedure AP 05-013, step 6.5, specified evaluation of vendor technical documentation,

but it did not specify how to disposition informal information. This step required a review

of vendor documentation by engineering to ensure design requirements are met.

Procedure AP 05-013, step 6.6, specified incorporating changes to vendor documents

that originate with Wolf Creek, but it did not specify that the vendor must be contacted for

changes that Wolf Creek has not evaluated.

Procedure AP 05-002, Dispositions and Change Packages, Revision 8, specified how

Wolf Creek prepares, documents, and implements modifications to plant equipment and

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Enclosure 2

design documents. Procedure AP 05-002, step 6.4.5, required that the data be obtained

from the vendor and placed in the modification package supporting the plant change.

Procedure AP 05-002, step 6.4.6.6, did not allow informal communications to form the

basis for a modification. Telephone calls are defined as informal communication per

Procedure AP 05-005. The inspectors found no documentation to show validation of the

verbal data provided by the vendor. This modification was a corrective action to

VIO 05000482/2009002-07 (EA-09-110). This notice of violation will remain open until

full compliance has been restored. Wolf Creek subsequently consulted with

Westinghouse to confirm the acceptability of the increased flow rate, and requested a

formal calculation. This issue is captured in Condition Report 22824.

Analysis. The inspectors found that the failure to follow procedure for the modification

was a performance deficiency. Traditional enforcement does not apply since there were

no actual safety consequences or potential for impacting the NRC's regulatory function,

and the finding was not the result of any willful violation of NRC requirements or Wolf

Creek procedures. The inspectors determined that this finding was more than minor

because this issue aligned with Inspection Manual Chapter 0612, Appendix E,

example 2.f, in that the modification relied on verbal statements to raise the allowable

flow through the heat exchanger. This is a significant deficiency in the modification

package. The inspectors determined this finding was associated with the design control

attribute of the Initiating Events Cornerstone and affected the cornerstone objective to

limit the likelihood of events that upset plant stability and challenge critical safety

functions. The inspectors evaluated the significance of this finding using Phase 1 of

Inspection Manual Chapter 0609.04 and determined that the finding was of very low

safety significance because assuming worst case degradation, the finding would not

result in exceeding the technical specification limit for identified reactor coolant system

leakage and would not have likely affected other mitigation systems resulting in a total

loss of their safety function because seal injection was available. This finding has a

crosscutting aspect in the area of human performance associated with work practices in

that management was unsuccessful in communicating expectations on procedure use

and adherence in engineering H.4.b].

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control," requires,

in part, that the licensee establish measures for the identification and control of design

interfaces and for coordination among participating design organizations. These

measures shall include the establishment of procedures among participating design

organizations for the review, approval, release, distribution, and revision of documents

involving design interfaces. It also requires, in part, that design changes shall be subject

to design control measures commensurate with those applied to the original design.

Procedures AP 05-005 and AP 05-002 implement this requirement by requiring formal

vendor data required for modifications to be incorporated into modifications. Contrary to

the above, from August 13, 2009, to December 31, 2009, Wolf Creek failed to obtain

vendor design data for configuration change Package 013096 in accordance with

Procedures AP 05-005 and AP 05-002. Because the finding is of very low safety

significance and has been entered into the corrective action program as Condition

Report 22824, this violation is being treated as a noncited violation, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-10, Failure to

Obtain Vendor Data Necessary for Plant Modification.

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Enclosure 2

1R19 Postmaintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

October 23, 2009, Emergency diesel generator A run after replacement of speed

switch

October 23, 2009, Instrumentation and control testing of emergency diesel

generator A instrument power supply

November 6, 2009, Essential service water train B pump and motor replacement

November 2, 2009, Motor-operated valve MOV 8811A after actuator and internals

replacement

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the USAR,

10 CFR Part 50 requirements, licensee procedures, and various NRC generic

communications to ensure that the test results adequately ensured that the equipment

met the licensing basis and design requirements. In addition, the inspectors reviewed

corrective action documents associated with postmaintenance tests to determine

whether the licensee was identifying problems and entering them in the corrective action

program and that the problems were being corrected commensurate with their

importance to safety. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of four postmaintenance testing inspection

samples as defined in Inspection Procedure IP 71111.19-05.

b.

Findings

No findings of significance were identified.

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Enclosure 2

1R20 Refueling and Other Outage Activities (71111.20)

a.

Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Wolf

Creek refueling outage, conducted from October 10 to November 17 2009, to confirm

that licensee personnel had appropriately considered risk, industry experience, and

previous site-specific problems in developing and implementing a plan that assured

maintenance of defense in depth. During the refueling outage, the inspectors observed

portions of the shutdown and cooldown processes and monitored licensee controls over

the outage activities listed below.

Configuration management, including maintenance of defense in depth, is

commensurate with the outage safety plan for key safety functions and

compliance with the applicable technical specifications when taking equipment

out of service.

Clearance activities, including confirmation that tags were properly hung and

equipment appropriately configured to safely support the work or testing.

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error.

Status and configuration of electrical systems to ensure that technical

specifications and outage safety-plan requirements were met, and controls over

switchyard activities.

Monitoring of decay heat removal processes, systems, and components.

Verification that outage work was not impacting the ability of the operators to

operate the spent fuel pool cooling system.

Reactor water inventory controls, including flow paths, configurations, and

alternative means for inventory addition, and controls to prevent inventory loss.

Controls over activities that could affect reactivity.

Maintenance of secondary containment as required by the technical

specifications.

Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage.

Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the drywell (primary containment) to verify that debris had not been

left which could block emergency core cooling system suction strainers, and

reactor physics testing.

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Enclosure 2

Licensee identification and resolution of problems related to refueling outage

activities.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one refueling outage and other outage

inspection sample as defined in Inspection Procedure IP 71111.20-05.

b.

Findings

.1

Introduction. The inspectors identified a Green cited violation of 10 CFR Part 50,

Appendix B, Criterion III, Design Control, for failure to correct a previous violation for an

inadequate vent path for the reactor vessel head.

Description. NRC Inspection Report 05000482/2008004 documented a Green noncited

violation of 10 CFR Part 50, Criterion III, Design Control, associated with the formation

of voids in the reactor vessel head during refueling outages.

During Refueling Outage 17 on October 13, 2009, Wolf Creek depressurized the reactor

and drained the reactor coolant system via the pressurizer to a level 374 inches above

the bottom of the hot leg. Reactor coolant system pressure was established at

atmospheric pressure, approximately 6-10 psig below the volume control tank pressure.

These actions were performed in accordance with plant operating

Procedure SYS BB-215, RCS Drain Down with Fuel in Reactor. The operators

completed Sections 6.1 and 6.2 of the procedure to vent the reactor vessel head to the

pressurizer and purge the pressurizer with nitrogen.

Control room operators subsequently initiated Condition Reports 20648 and 20633 to

identify anomalous readings in pressurizer and reactor vessel level. The inspectors

reviewed plant computer data from October 11 to 14, 2009, and confirmed that a void

had formed in the reactor vessel head region following reactor coolant system

depressurization. As the gas built up, it forced primary coolant out of the reactor vessel

and into the pressurizer over many hours, causing the observed level changes.

Following the previous refueling outage, Wolf Creek Mode 5 Procedure GEN 00-009 had

been changed to require reactor vessel level instrumentation system to be in service so

that control room operators could observe any decrease in reactor vessel level. Based

on plant computer data, the observed change of approximately 41 inches in pressurizer

level equated to a maximum void size of 1100 gallons of primary coolant in the reactor

vessel. Excluding the void, time to boil in the reactor coolant system was calculated to

be 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> during outage planning.

Following the formation of a similar void in Refueling Outage 16, Wolf Creek initiated a

root cause evaluation during under Condition Report 2008-001032. The void size during

Refueling Outage 16 was 2600 gallons. Wolf Creek determined that the root cause was

a loop seal or blockage in the piping. The root cause described boron precipitation as a

possible source of the blockage. Corrective actions were subsequently planned for

Refueling Outage 17. The slope of the vessel head piping was verified to be correct to

ensure no loop seals was performed as a corrective action to prevent recurrence.

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Enclosure 2

However, after the piping slope was verified and loop seals ruled out as a possible

cause, no additional actions were taken to identify the cause of the inadequate vent. A

corrective action to perform an internal inspection of the vessel head was not performed

because Wolf Creek did not have tools to inspect around 90 bends in the piping. The

inspectors determined that Wolf Creek failed to identify the cause of the inadequate vent

path to relieve gases to the pressurizer, with the result that voiding would continue to be

a concern in the next refueling outage.

When the NRC issued NCV 05000482/2008004-07 on November 7, 2008, for the

reactor vessel head voiding during outages, corrective actions were tracked under

Condition Report 2008-001032. The inspectors concluded that Wolf Creek has yet to

correct the inadequate vent path, allowing void formation to continue to occur in the

reactor vessel head. Without an adequate vent from the top of the reactor vessel head

to the pressurizer, noncondensable gas voids will form, decreasing reactor coolant

inventory and reducing the time to core boiling following a loss of shutdown cooling. The

gas voids could grow to the top of the hot legs or until the driving head forces the void

past the blockage and into the gas space of the pressurizer, causing the plant to

inadvertently enter mid-loop operations. An adequate vent path is necessary to control

reactor coolant level. Wolf Creek has initiated a second root cause under Condition

Report 22501.

Analysis. The inspectors determined that failure to provide an adequate vessel head

vent path to prevent gas accumulation in the reactor vessel during depressurized plant

operations was a performance deficiency. The inspectors determined that this finding

was associated with the design control attribute of the Initiating Events Cornerstone.

Specifically, the voiding reduces time to boil and impacted the cornerstone objective to

limit the likelihood of those events that upset plant stability and challenge critical safety

functions during shutdown as well as power operations. The inspectors evaluated the

significance of this finding using Inspection Manual Chapter 0609, Appendix G,

Attachment 1, Shutdown Operations Significance Determination Process Phase 1

Operational Checklists for Both PWRs and BWRs. The inspectors determined that

Checklist 3 was applicable because the unit was in cold shutdown with the refueling

cavity level less than 23 feet. Based upon Appendix G, Attachment 1, Checklist 3,

Phase 2, analysis was not needed to characterize the risk significance of this finding

because the level of loss was less than two feet, did not occur during reduced inventory,

and appropriate action was taken regarding the level deviation. The finding was

determined to be of very low safety significance based upon the demonstrated

availability of mitigation systems and the reactor coolant system cavity inventory. The

inspectors determined the cause of the finding had a problem identification and

resolution aspect in the corrective action program. Specifically, Wolf Creeks corrective

actions were not successful to address the vent path blockage in a timely manner

P.1(d).

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,

in part, that the design basis is correctly translated into specifications, drawings, and

procedures. The design basis of the reactor vessel head vent is to allow

noncondensable gases to escape to the pressurizer during shutdown conditions.

Contrary to the above, from December 2, 2003, to December 31, 2009, Wolf Creek

- 50 -

Enclosure 2

failed to ensure the design basis of the reactor vessel head vent was correctly translated

into specifications, drawings, and procedures. Specifically, Wolf Creek designed and

installed a reactor vessel head permanent vent piping modification which failed to vent

noncondensable gases to the pressurizer during shutdown operations. This resulted in

the formation of voids in the reactor vessel head while the plant was shutdown and

depressurized in successive refueling outages. This issue and the corrective actions are

being tracked by the licensee in Condition Reports 22501, 20648, 20568, and 20633.

Due to the licensees failure to restore compliance from previous

NCV 05000482/2008004-07 within a reasonable time after the violation was identified,

this violation is being cited as a Notice of Violation consistent with Section VI.A of the

Enforcement Policy: VIO 05000482/2009005-11, Failure to Correct Vessel Head Vent

Path (EA-10-020).

.2

Introduction. The inspectors identified a Green noncited violation of Technical

Specification 5.4.1.a for failure to properly implement Procedure AP 14A-003, Scaffold

Construction and Use, when scaffolding was erected against operable safety-related

equipment.

Description. On October 15, 2009, the inspectors identified scaffolding in contact with

component cooling water piping inside containment. The piping was the containment

loop which did not have any required cooling loads, but was part of an operating

component cooling water train that was cooling the core. At the time, reactor coolant

system level was below the vessel flange. The tag on the scaffold explicitly stated that it

was not seismically qualified. The inspectors discussed the issue with the shift manager

who immediately had the scaffold moved. Both steam generators were inoperable and

both trains of residual heat removal were required to be operable. The inspectors

reviewed the bases for Technical Specification 3.4.7, RCS Loops - Mode 5, Loops

Filled, which required an operable heat sink path from residual heat removal to

component cooling water to essential service water.

Procedure AP 14A-003, Scaffold Construction and Use, step 6.4.15, required

scaffolding to be two inches away from equipment. Attachment F of this procedure

specifies the requirements for seismically qualified scaffolds. The scaffold form stated

that the scaffolding was required to be removed prior to Mode 4, which was incorrect

because it allowed nonseismically qualified scaffold to be installed in the zone of

influence of operable equipment since seismic qualification is still required for equipment

required to be operable in Modes 5 and 6. This issue was entered into the corrective

action program as Condition Report 22464.

Analysis. The construction of an unqualified scaffold against operable component

cooling water piping was a performance deficiency. Traditional enforcement does not

apply since there were no actual safety consequences or potential for impacting the

NRC's regulatory function, and the finding was not the result of any willful violation of

NRC requirements or Wolf Creek procedures. The inspectors determined that this

finding was more than minor because it is associated with the equipment performance

attribute for the Mitigating Systems Cornerstone, and it affected the cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences (i.e., core damage). Specifically,

- 51 -

Enclosure 2

this issue relates to the availability and reliability examples of the equipment

performance attribute because a latent failure mechanism was not evaluated. The

inspectors evaluated the significance of this finding using Inspection Manual

Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance

Determination Process Phase 1 Operational Checklists for Both PWRs and BWRs. The

inspectors determined that Checklist 3 was applicable because the unit was in cold

shutdown with the refueling cavity level less than 23 feet. Using Appendix G,

Attachment 1, Checklist 3, Phase 2 analysis was not needed and the finding was of very

low safety significance (Green) because the licensee was able to demonstrate that the

seismically unqualified scaffolding would not have resulted in a loss of safety function.

The inspectors determined the cause of the finding had a human performance aspect in

the area of resources. Specifically, Procedure AP 14A-003 was inadequate because it

had conflicting guidance that allowed seismically unqualified scaffolds in Modes 5 and 6

H.2.c].

Enforcement. Technical Specification 5.4.1.a requires that procedures be established,

implemented and maintained as recommended in Regulatory Guide 1.33, Appendix A.

Section 9.a of Appendix A, requires, in part, that maintenance affecting safety-related

equipment be accomplished in accordance with procedures. Procedure AP 14A-003

Scaffold Construction and Use, Revision 16, step 6.4.15 required two inches of

clearance from safety-related structures. Contrary to the above, from October 14 to 15,

2009, the licensee did not provide two inches of clearance between scaffolding and

safety-related structures. Specifically, component cooling water Train B was in contact

with a seismically unqualified scaffold while component cooling water was required to be

operable. Because the finding is of very low safety significance and has been entered

into the corrective action program as Condition Report 22464, this violation is being

treated as a noncited violation, consistent with Section VI.A of the NRC Enforcement

Policy: NCV 05000482/2009005-12, Unevaluated Scaffold Against Component Cooling

Water Piping.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors reviewed the USAR, procedure requirements, and technical

specifications to ensure that the seven surveillance activities listed below demonstrated

that the systems, structures, and/or components tested were capable of performing their

intended safety functions. The inspectors either witnessed or reviewed test data to verify

that the significant surveillance test attributes were adequate to address the following:

Preconditioning

Evaluation of testing impact on the plant

Acceptance criteria

Test equipment

- 52 -

Enclosure 2

Procedures

Jumper/lifted lead controls

Test data

Testing frequency and method demonstrated technical specification operability

Test equipment removal

Restoration of plant systems

Fulfillment of ASME Code requirements

Updating of performance indicator data

Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

Reference setting data

Annunciators and alarms setpoints

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

October 28, 2009, MOV 8811A as-found inservice surveillance test

August 10, 2009, STS IC-250B, Channel operational test containment

atmosphere and reactor coolant system leak rate radiation Monitor GT RE-0031

November 5, 2009, STS PE-139, Local leak rate test of Penetration 39,

BB HV-351C

September 17, 2009, Train A auxiliary feedwater inservice testing of

Valves ALV0002 and ALV0009

November 3, 2009, Essential service water Train B leak test of underground pipe

September 28, 2009, Emergency Diesel Generator A, 24-hour endurance run

October 15, 2009, Emergency Diesel Panel KJ-122/123 safety to nonsafety fuse

inspections

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of seven surveillance testing inspection samples

as defined in Inspection Procedure IP 71111.22-05.

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Enclosure 2

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a.

Inspection Scope

This area was inspected to assess licensee personnels performance in implementing

physical and administrative controls for airborne radioactivity areas, radiation areas, high

radiation areas, and worker adherence to these controls. The inspectors used the

requirements in 10 CFR Part 20, the technical specifications, and the licensees

procedures required by technical specifications as criteria for determining compliance.

During the inspection, the inspectors interviewed the radiation protection manager,

radiation protection supervisors, and radiation workers. The inspectors performed

independent radiation dose rate measurements and reviewed the following items:

Performance indicator events and associated documentation packages reported

by the licensee in the Occupational Radiation Safety Cornerstone

Controls (surveys, posting, and barricades) of radiation, high radiation, or

airborne radioactivity areas

Radiation work permits, procedures, engineering controls, and air sampler

locations

Conformity of electronic personal dosimeter alarm set points with survey

indications and plant policy; workers knowledge of required actions when their

electronic personnel dosimeter noticeably malfunctions or alarms

Barrier integrity and performance of engineering controls in airborne radioactivity

areas

Physical and programmatic controls for highly activated or contaminated

materials (nonfuel) stored within spent fuel and other storage pools

Self-assessments, audits, licensee event reports, and special reports related to

the access control program since the last inspection

Corrective action documents related to access controls

Licensee actions in cases of repetitive deficiencies or significant individual

deficiencies

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Enclosure 2

Radiation work permit briefings and worker instructions

Adequacy of radiological controls, such as required surveys, radiation protection

job coverage, and contamination control during job performance

Dosimetry placement in high radiation work areas with significant dose rate

gradients

Changes in licensee procedural controls of high dose rate - high radiation areas

and very high radiation areas

Controls for special areas that have the potential to become very high radiation

areas during certain plant operations

Posting and locking of entrances to all accessible high dose rate - high radiation

areas and very high radiation areas

Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

Either because the conditions did not exist or an event had not occurred, no

opportunities were available to review the following items:

Adequacy of the licensees internal dose assessment for any actual internal

exposure greater than 50 millirem committed effective dose equivalent

These activities constitute completion of 21 of the required 21 samples as defined in

Inspection Procedure IP 71121.01-05.

b.

Findings

.1

Introduction. The inspector identified a Green noncited violation of

Technical Specification 5.7.2.a.1 for failure to maintain administrative control of door

and gate keys to high radiation areas with dose rates greater than 1 rem per hour but

less than 500 rads per hour (referred to as locked high radiation areas).

Description. During a review of the licensees program for administrative control of

keys to doors and gates to locked high radiation areas and very high radiation areas, the

inspector found that the health physics department had a master key to locked high

radiation areas. This key was not controlled in accordance with licensee

Procedure AP 25A-200, Access to Locked High or Very High Radiation Areas,

Revision 20, which stated that site security was responsible for issuing locked high

radiation area and very high radiation area keys. In accordance with technical

specifications, health physics management designated the site security department to

administratively (and procedurally) control the keys. Although site security was

effectively meeting the procedure requirement for issuing all other locked and very high

- 55 -

Enclosure 2

radiation area keys, site security was unaware that the health physics department had

the only master key to locked high radiation areas at the site. By procedure, site security

administratively controlled the other keys (to locked and very high radiation areas) by

maintaining an inventory of them, performing physical inventories of the keys each shift,

and labeling the keys. None of these administrative controls were implemented for the

master key in the health physics department. The licensee immediately documented the

deficiency in a condition report and implemented temporary administrative controls until

a permanent disposition for the master key had been identified.

Analysis. Failure to maintain administrative control of the master key to locked high

radiation areas was a performance deficiency. This finding is greater than minor because if

left uncorrected the finding has the potential to lead to a more significant safety concern in

that an individual could receive unanticipated radiation dose by gaining access a locked high

radiation area without the proper controls and briefing. This finding was evaluated using

Inspection Manual Chapter 0609, Significance Determination Process, Appendix C,

Occupational Radiation Safety Significance Determination Process, and was determined to

be of very low safety significance because it did not involve: (1) an as low as is reasonably

achievable (ALARA) planning or work control issue, (2) an overexposure, (3) a substantial

potential for overexposure, or (4) an impaired ability to assess dose. Additionally, the

violation has a crosscutting aspect in the area of human performance associated with the

work practices component because the lack of peer and self-checking resulted in

inadequate control of keys to locked high radiation areas H.4(a).

Enforcement. Technical Specification 5.7.2.a.1 requires, in part, that each entryway to a

high radiation area with dose rates greater than 1.0 rem per hour but less than 500 rads

per hour shall be provided with a locked or continuously guarded door or gate that

prevents unauthorized entry and all keys shall be maintained under the administrative

control of the shift manager/control room supervisor, health physics supervision, or

his/her designee. Contrary to the above, as of October 21, 2009, the licensee failed to

maintain administrative control of a master key to high radiation areas with dose rates in

excess of 1.0 rem per hour but less than 500 rads per hour. Because this violation was

of very low safety significance and has been entered into the licensee's corrective action

program as Condition Report 20973, it is being treated as a noncited violation consistent

with Section VI.A of the NRC Enforcement Policy: NCV 05000482/2009005-13, Failure

to Maintain Administrative Control of Keys to Locked High Radiation Areas.

2OS2 ALARA Planning and Controls (71121.02)

a.

Inspection Scope

The inspectors assessed licensee personnels performance with respect to maintaining

individual and collective radiation exposures as low as is reasonably achievable. The

inspectors used the requirements in 10 CFR Part 20 and the licensees procedures

required by technical specifications as criteria for determining compliance. The

inspectors interviewed licensee personnel and reviewed the following:

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Enclosure 2

Five outage or on-line maintenance work activities scheduled during the

inspection period and associated work activity exposure estimates which were

likely to result in the highest personnel collective exposures

Site-specific ALARA procedures

ALARA work activity evaluations, exposure estimates, and exposure mitigation

requirements

Interfaces between operations, radiation protection, maintenance, maintenance

planning, scheduling and engineering groups

Shielding requests and dose/benefit analyses

Dose rate reduction activities in work planning

Use of engineering controls to achieve dose reductions and dose reduction

benefits afforded by shielding

Workers use of the low dose waiting areas

First-line job supervisors contribution to ensuring work activities are conducted in

a dose efficient manner

Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

Self-assessments, audits, and special reports related to the ALARA program

since the last inspection

Corrective action documents related to the ALARA program and follow-up

activities, such as initial problem identification, characterization, and tracking

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of 6 of the required 15 samples and 6 of the

optional samples as defined in Inspection Procedure IP 71121.02-05.

b.

Findings

No findings of significance were identified.

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Enclosure 2

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1

Data Submission Issue

a.

Inspection Scope

The inspectors performed a review of the data submitted by the licensee for the 3rd

Quarter 2009 performance indicators for any obvious inconsistencies prior to its public

release in accordance with Inspection Manual Chapter 0608, Performance Indicator

Program.

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b.

Findings

No findings of significance were identified.

.2

Mitigating Systems Performance Index - Emergency ac Power System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Emergency ac Power System performance indicator data for the period from the

4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in Revision 6 of the Nuclear Energy Institute (NEI)

Document 99-02, Regulatory Assessment Performance Indicator Guideline, were

used. The inspectors reviewed the licensees operator narrative logs, mitigating systems

performance index derivation reports, issue reports, event reports, and NRC integrated

inspection reports for the period of October 1, 2008, through September 30, 2009, to

validate the accuracy of the submittals. The inspectors reviewed the mitigating systems

performance index component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the

performance indicator data collected or transmitted for this indicator and none were

identified. Specific documents reviewed are described in the attachment to this report.

This inspection constitutes one mitigating systems performance index - emergency ac

power system sample as defined by Inspection Procedure IP 71151.

b.

Findings

No findings of significance were identified.

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Enclosure 2

.3

Mitigating Systems Performance Index - High Pressure Injection Systems

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - High Pressure Injection Systems performance indicator data for the period from

the 4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in Revision 6 of the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, were used. The inspectors

reviewed the licensees operator narrative logs, issue reports, mitigating systems

performance index derivation reports, event reports, and NRC integrated inspection

reports for the period of October 1, 2008, through September 30, 2009, to validate the

accuracy of the submittals. The inspectors reviewed the mitigating systems performance

index component risk coefficient to determine if it had changed by more than 25 percent

in value since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the performance

indicator data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the attachment to this report.

This inspection constitutes one mitigating systems performance index - high pressure

injection system sample as defined by Inspection Procedure IP 71151.

b.

Findings

No findings of significance were identified.

.4

Mitigating Systems Performance Index - Auxiliary Feedwater System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Auxiliary Feedwater System performance indicator data for the period from the

4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in Revision 6 of the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, were used. The inspectors

reviewed the licensees operator narrative logs, issue reports, event reports, mitigating

systems performance index derivation reports, and NRC integrated inspection reports

for the period of October 1, 2008, through September 30, 2009, to validate the accuracy

of the submittals. The inspectors reviewed the mitigating systems performance index

component risk coefficient to determine if it had changed by more than 25 percent in

value since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the performance

indicator data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the attachment to this report.

- 59 -

Enclosure 2

This inspection constitutes one mitigating systems performance index - auxiliary

feedwater sample as defined by Inspection Procedure IP 71151.

b.

Findings

No findings of significance were identified.

.5

Mitigating Systems Performance Index - Residual Heat Removal System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Residual Heat Removal System performance indicator data for the period from

the 4th quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in Revision 6 of the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, were used. The inspectors

reviewed the licensees operator narrative logs, issue reports, mitigating systems

performance index derivation reports, event reports, and NRC integrated inspection

reports for the period of October 1, 2008, through September 30, 2009, to validate the

accuracy of the submittals. The inspectors reviewed the mitigating systems

performance index component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the

performance indicator data collected or transmitted for this indicator and none were

identified. Specific documents reviewed are described in the attachment to this report.

This inspection constitutes one Mitigating Systems Performance Index - Residual Heat

Removal System sample as defined by Inspection Procedure IP 71151.

b.

Findings

No findings of significance were identified.

.6

Mitigating Systems Performance Index - Cooling Water Systems

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Cooling Water Systems performance indicator data for the period from the 4th

quarter 2008 through the 3rd quarter 2009. To determine the accuracy of the

performance indicator data reported during those periods, performance indicator

definitions and guidance contained in Revision 6 of the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, were used. The inspectors

reviewed the licensees operator narrative logs, issue reports, mitigating systems

performance index derivation reports, event reports, and NRC integrated inspection

reports for the period of October 1, 2008, to September 30, 2009, to validate the

- 60 -

Enclosure 2

accuracy of the submittals. The inspectors reviewed the mitigating systems

performance index component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the

performance indicator data collected or transmitted for this indicator and none were

identified. Specific documents reviewed are described in the attachment to this report.

This inspection constitutes one mitigating systems performance index - cooling water

system sample as defined by Inspection Procedure IP 71151.

b.

Findings

No findings of significance were identified.

.7

Occupational Exposure Control Effectiveness (OR01)

a.

Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences performance indicator for the period from the 4th quarter 2008 through 3rd

quarter 2009. To determine the accuracy of the performance indicator data reported

during those periods, performance indicator definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,

was used. The inspectors reviewed the licensees assessment of the performance

indicator for occupational radiation safety to determine if indicator related data was

adequately assessed and reported. To assess the adequacy of the licensees

performance indicator data collection and analyses, the inspectors discussed with

radiation protection staff, the scope and breadth of its data review, and the results of

those reviews. The inspectors independently reviewed electronic dosimetry dose rate

and accumulated dose alarm and dose reports and the dose assignments for any

intakes that occurred during the time period reviewed to determine if there were

potentially unrecognized occurrences. The inspectors also conducted walkdowns of

numerous locked high and very high radiation area entrances to determine the adequacy

of the controls in place for these areas.

These activities constitute completion of the occupational radiological occurrences

sample as defined in Inspection Procedure IP 71151-05.

b.

Findings

No findings of significance were identified.

- 61 -

Enclosure 2

.8

Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (PR01)

a.

Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent Technical

Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences

performance indicator for the period from the 4th quarter 2008 through 3rd quarter 2009.

To determine the accuracy of the performance indicator data reported during those

periods, performance indicator definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,

was used. The inspectors reviewed the licensees issue report database and selected

individual reports generated since this indicator was last reviewed to identify any

potential occurrences such as unmonitored, uncontrolled, or improperly calculated

effluent releases that may have impacted offsite dose.

These activities constitute completion of the radiological effluent technical

specifications/offsite dose calculation manual radiological effluent occurrences sample

as defined in Inspection Procedure IP 71151-05.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical

Protection

.1

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included: the complete and

accurate identification of the problem; the timely correction, commensurate with the

safety significance; the evaluation and disposition of performance issues, generic

implications, common causes, contributing factors, root causes, extent of condition

reviews, and previous occurrences reviews; and the classification, prioritization, focus,

and timeliness of corrective actions. Minor issues entered into the licensees corrective

action program because of the inspectors observations are included in the attached list

of documents reviewed.

- 62 -

Enclosure 2

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by inspection procedure, they were

considered an integral part of the inspections performed during the quarter and

documented in Section 1 of this report.

b.

Findings

No findings of significance were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for followup, the inspectors performed a daily screening of

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b.

Findings

No findings of significance were identified.

.3

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensees corrective action program and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors focused their review on repetitive equipment

issues, but also considered the results of daily corrective action item screening

discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human

performance results. The inspectors nominally considered the 6-month period of

June 30 through December 31, 2009, although some examples expanded beyond those

dates where the scope of the trend warranted.

The inspectors also included issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and maintenance rule assessments.

The inspectors compared and contrasted their results with the results contained in the

licensees corrective action program trending reports. Corrective actions associated with

a sample of the issues identified in the licensees trending reports were reviewed for

adequacy.

These activities constitute completion of one single semi-annual trend inspection sample

as defined in Inspection Procedure IP 71152-05.

- 63 -

Enclosure 2

b.

Findings

No findings of significance were identified.

.4

Selected Issue Follow-up Inspection

a.

Inspection Scope

The inspectors selected two issues for follow-up inspection per Inspection

Procedure IP 71152. During a review of items entered in the licensees corrective action

program, the inspectors recognized a corrective action item documenting a problem with

extraction steam on June 23, 2009, that caused an increase in reactivity. The inspectors

reviewed corrective actions and new procedure changes for level control of high

pressure feedwater heaters. The inspectors also reviewed several condition reports and

interviewed personnel pertaining to the intermediate range nuclear instrument NI-36.

The deficiencies associated with NI-36 constituted one in-depth review of an operator

work-around.

These activities constitute completion of two in-depth problem identification and

resolution samples as defined in Inspection Procedure IP 71152-05.

b.

Findings

Introduction. On December 30, 2009, the inspectors identified a Green noncited

violation of Technical Specification, Table 3.3.1-1, Function 18.a, when Wolf Creek

restarted from on May 18, 2005.

Description. On April 9, 2005, Wolf Creek shut down for Refueling Outage 14. The

inspectors found no control room log entries stating that source range instrument NI-32

had to be manually energized. The inspectors reviewed a completed copy of

STN IC-236, Revision 4, dated April 9, 2005, which stated that compensation voltage

and current were found within tolerance and were left as-found. At the end of Refueling

Outage 14, in Mode 3, NI-36 indication deviated from indication from intermediate range

detector NI-35. During interviews with licensed operators, when shutdown banks were

withdrawn, NI-36 went above 6 E-11 amps and cleared the P-6 interlock while the

reactor was subcritical. Indication above 6E-11 normally means the reactor is critical.

The source ranges count rates and NI-35 also increased, but did not indicate criticality.

Troubleshooting was performed under Work Order 05-272906-000 was performed on

May 16, 2005. Instrumentation and controls technicians disconnected, cleaned, and

reconnected NI-36 cables. The NI-36 cables were then disconnected and reconnected

two more times. Work Order 05-272906-000 was also used to perform STS IC-436,

Channel Calibration NIS Intermediate Range N-36, Revision 15, test the log current

amplifier and indicator calibrations, Work Order 05-272906-000 was also used to

perform STN IC-236, Intermediate Range N36 Compensation Voltage Adjustment,

Revision 4 to calibrate the compensating voltage power supply and test the loss of

compensating voltage bistable relay driver. On May 17, 2005, during calibration of the

compensating voltage, during step 8.2.4.1, the technicians noted that compensating

- 64 -

Enclosure 2

voltage was not changing indication permanently, only temporarily. The as-found and

as-left compensating voltage were satisfactory, but the compensating current as-found

and as-left was at 1E-10amps which is one order of magnitude above the 3E-11amps

acceptance criteria. The surveillance was closed stating used only as troubleshooting

tool only. No credit taken. The surveillance test routing sheet noted this as a technical

specification failure. This was then used to generate Work Order 05-272906-000 which

stated that there was a possible problem with the signal cable for NI-32 and the

compensation cable for NI-36 and to rework the cables. The operators had to remove

instrument fuses from the NI-36 instrument rack to cause the interlock to clear after the

efforts below. During control rod pulls during preparations for criticality, the P-6 interlock

came in with the reactor subcritical. Fuses had to later be pulled and re-inserted to clear

the interlock after NI-36 was worked during this series of work orders.

Using Work Order 05-272926-005, the technicians used STS IC-236 to successfully test

the positive and negative 25 Vdc power supplies, the high voltage power supply, the

power above permissive P-6 bistable relay driver, and the reactor trip high level

bistable relay driver. However, other than disconnecting cleaning, and reconnecting the

connectors, no corrective maintenance was performed on cables. The cause of the

failure was documented as suspect loose connection. Wolf Creek concluded that after

the above efforts, that NI-36 indication had been reduced sufficiently to declare it

operable because it channel checked with NI-35 to within one decade. Reactor startup

commenced on May 18, 2005, and concluded Refueling Outage 14.

During a reactor shutdown for Refueling Outage 15 on October 7, 2006, intermediate

range neutron Detector NI-36 did not decrease below 6E -11 amps and energize source

range detector NI-32. Following NI-36s failure to decrease below the P-6 setpoint,

reactor operators correctly transitioned to Procedure OFN SB-008, Instrument

Malfunctions to manually energize source range detector NI-32. On October 7, 2006,

Wolf Creek performed STN IC-236 under Work Order 05-274604-000. Detector NI-36

failed STN IC-236, Intermediate Range N36 Compensation Voltage Adjustment,

Revision 4, because the as-found detector current was outside of the tolerance range at

9E-11 amps (upper limit is 3E-11 amps) and could not be adjusted to within the

tolerance. As-found compensating voltage was within the allowable range.

Wolf Creek then replaced the jacks for the triaxial connector using Work

Order 05-272987-000. Work Order 05-272987-000 stated that the connector was found

failed but did not state what acceptance criteria it did not meet. Work

Order 05-272987-000 stated that the cause of the failure was suspect failed connector.

Also, Work Order 05-272987-000 took measurements of the compensation voltage cable

insulation resistance testing, but stated no acceptance criteria. Work Order 05-272987-

000 the performed surveillance test STS IC-236, Channel Operational Test Nuclear

Instrumentation System Intermediate Range N-36 Protection Set II, Revision 17, which

was followed by Work Order 06-289017-000 to perform STN IC-236. On October 17,

2006, STN IC-236 adjusted the compensating voltage to be more positive. The as-found

adjustment of the detector current was less than 1E-11amps, which was outside the

STN IC-236 acceptance criteria. The inspectors noted that the instrument drawer will

not allow detector current to decrease below 1E-11 amps due to a designed idling

current at 1E-11 amps. As-left current was 1E-11 amps. Later in the outage, control

- 65 -

Enclosure 2

room operators requested that instrumentation and control workers adjust NI-36

because its output was not tracking with the other intermediate range detector, NI-35.

On November 9, 2006, STN IC-236 was performed again. During this test,

compensation current was unable to be adjusted below 3E-11 amps. The as-found

value was 7E-11 amps and the as-left value was 6E-11 amps. The 6E-11 amp current

was outside the allowable limit, but the surveillance procedure was completed with a

deficiency stating no credit taken. The surveillance cover sheet said that NI-36 was

reading within an order of magnitude of NI-35. The control room logs stated the same.

Work Order 06-290208-000 was generated to replace the detector during the Refueling

Outage 16.

On March 17, 2008, Wolf Creek tripped from 100 percent power and NI-36 automatically

energized source range detector NI-32. The inspectors checked plant computer data

and found that the source range instrument energized at 5E-11 amps which is below the

acceptance criteria of greater than 6 E-11amps (P-6 setpoint). The detector was

subsequently replaced during Refueling Outage 16.

The need to transition to Procedure EMG FR-S2, Response to Loss of Core Shutdown,

was not previously identified in a condition report, operator work around, or operator

burden. The inspectors found no other evaluation of the detectors behavior before Wolf

Creek ascended to Mode 2 in Refueling Outages 14 and 15. The inspectors found that

the connector cleaning in Refueling Outage 14 and the jack replacement in Refueling

Outage 15 were not likely to correct the problem found in STN IC-236. The inspectors

concluded that the STN IC-236 surveillances in Refueling Outage 14 and Refueling

Outage 15 had not met the acceptance criteria and that startup should not have

continued until the nuclear instrument issue was resolved. Wolf Creek did not identify

the issue as a technical specification violation. Although work orders were planned in

Refueling Outage 14 to replace NI-36, all were closed without action. The inspectors

found that NI-36 was conditioned through troubleshooting until it could pass its one

decade channel check. Other testing performed by Wolf Creek only impacted the

instrument drawer in the control room, while the problem was related to the detector

itself. Condition Report 2006-003187 found that the problems with compensating

voltage could not be determined, but concluded that it was not necessary for operability

because the system had no risk significance. The inspectors determined that the

compensation current is critical to the operation of the detectors because the design of

the compensated ion chamber is to allow the instrument drawer to sum currents in

opposing directions to discriminate neutrons from gamma. The condition report also

identified that the P-6 interlock may not work correctly, but no action was taken.

The inspectors reviewed Wolf Creek Technical Specification 3.3.1, Function 18.a,

Intermediate Range Flux, P-6 [interlock], and its bases statement. The bases state

that Function 18.a ensures that, on decreasing power, the P-6 interlock automatically

energizes nuclear instrumentation source range detectors and enables the source range

neutron flux reactor trip. During reactor trip, the function is required as reactor power

decreases to energize the source range detectors and the source range reactor trips.

The inspectors found that Wolf Creeks bases are consistent with the NUREG-1431,

Standard Technical Specifications Westinghouse Plants, Revision 3.0.

- 66 -

Enclosure 2

Analysis. The inspectors determined that the failure to ensure that the P-6 interlock was

operable per the technical specification as defined in the bases was a performance

deficiency. The finding was more than minor because it was associated with the

configuration control (reactivity control) attribute of the Barrier Integrity Cornerstone, and

it affected the cornerstone objective to provide reasonable assurance that physical

design barriers (fuel cladding, reactor coolant system, and containment) protect the

public from radionuclide releases caused by accidents or events. The inspectors

evaluated the significance of this finding under the Mitigating Systems Cornerstone

using Phase 1 of Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, and determined that the finding screened to Green

because the P-6 interlock only affected the fuel barrier. This finding was not assigned a

crosscutting aspect because the cause was not representative of current performance.

Enforcement. Wolf Creek Technical Specification, Table 3.3.1-1, Function 18.a,

requires, in part, that when intermediate range instrument measured neutron flux

decreases below the allowable value of greater than or equal to 6 E-11 amps that the

source range instruments be energized and enable the source range reactor trip signal.

Technical Specification, Table 3.3.1-1, Function 4, requires the intermediate range

detectors to be operable at low power in Modes 1 and 2. These functions are required

on reactor trip. Contrary to the above, from May 17, 2005, to March 17, 2008,

intermediate range detector NI-36 was inoperable because its output did not decrease

below the P-6 setpoint when the reactor tripped and failed to energize source range

instrument NI-32 and the source range reactor trip. Because this violation was

determined to be of very low safety significance and was placed in the corrective action

program as Condition Report 00022450, this violation is being treated as a noncited

violation in accordance with Section VI.A.1 of the Enforcement Policy: NCV 05000482/2009005-14, Failure to Identify Inoperable P-6 Interlock and Intermediate

Range Detector.

4OA3 Event Follow-up (71153)

.1

Response to Notice of Unusual Event

On October 22, 2009, Emergency Diesel Generator B was out of service for planned

maintenance. At 12:06 p.m., the Wolf Creek control room received trouble annunciators

for Emergency Diesel Generator A. The speed sensor failed high which would cause

any diesel start to fail. This stopped the jacket water keep warm pump, and prevented

air start system solenoids from starting the engine. Since the engine was in standby, low

lube oil pressure also would have prevented the engine from starting. Wolf Creek

initiated troubleshooting and repair. At 5:39 p.m., Wolf Creek declared an Unusual Event

under Emergency Action Level (EAL) 6/AC5 for loss of both diesels with the reactor

defueled. At 5:45 p.m., Wolf Creek made notification to state and local governments of

the Notice of Unusual Event. At 7:14 p.m., Wolf Creek notified the NRC Operations

Officer that the power supply had excessive voltage ripple which caused the speed

sensors failure. The speed switch and its power supply were replaced. The inspectors

observed control room activities, repair activities, and post-maintenance testing of

repairs. On October 23, 2009, at 7:38 a.m., Emergency Diesel Generator A was

restored to operable status and the unusual event was terminated.

- 67 -

Enclosure 2

b.

Findings

One violation of very low safety significance (Green) is described in Section 4OA7 of this

report.

.2

Licensee Event Report Review

a.

Inspection Scope

The inspectors reviewed potentially reportable events under Inspection

Procedure IP 71153. Inspectors also utilized NUREG 1022, Event Reporting Guidelines

10 CFR 50.72 and 50.73, Revision 2.

b.

Findings

Introduction. The inspectors identified a Severity Level IV noncited violation of

10 CFR 50.73, in which the licensee failed to submit licensee event reports within 60

days following discovery of events or conditions meeting the reportability criteria.

Description. The licensee submitted Licensee Event Report LER 2009-009-00 under

10 CFR 50.73(a)(2)(i)(B) for an operation prohibited by technical specifications. The

inspectors determined this event report was not submitted within the 60 days allowed by

10 CFR 50.73. The inspectors identified that other reporting requirements of 50.73 also

applied but were not included in the licensee event report.

In the event on August 22, 2009, Wolf Creek disabled both trains of the P-4 interlock for

planned maintenance. Specifically, the feedwater isolation signal that is generated by

P-4 (reactor trip coincident with low Tave) was taken out of service for control rod drive

motor-generator set testing. This allowed reactor trip breaker cycling without isolation of

main feedwater. The P-4 interlock was required by Technical Specification 3.3.2 function

8.a. This function is discussed in USAR Section 7.3.8, NSSS Engineered Safety

Feature Actuation System. which describes the function of a main feedwater isolation as

to prevent or mitigate the effect of an excessive cooldown. Wolf Creek technical

specification Bases also state that one or more functions may backup other engineered

safety feature actuation signal functions credited in Chapter 15 of the USAR.

Licensee Event Report 2009-009-00 reported a condition prohibited by technical

specifications under a(2)(i)(B) and correctly described that the P-4 interlock was not

credited in accident analysis. The licensee did not report the event under reporting

criteria 50.73(a)(2)(v). The engineered safety features actuation signal system has other

signals that cause feedwater isolations that are used in Chapter 15 of the USAR.

The inspectors consulted NUREG 1022, Event Reporting Guidelines 10 CFR 50.72

and 50.73, Revision 2. NUREG 1022, Section 3.2.7, reportability under 50.73(a)(2)(v),

specified that inoperable systems required by the technical specifications are to be

reported, even if there are other diverse, operable means of accomplishing the safety

function. The inspectors found that Wolf Creek was not correct in concluding that the

50.73(a)(2)(v)(A) through (D) only applied to the accident analysis contained in

Chapter 15 of the USAR. The inspectors consulted with the NRC Office of Nuclear

- 68 -

Enclosure 2

Reactor Regulation, who agreed with the inspectors application of the rule and

NUREG 1022. The untimely licensee event report was entered into the corrective action

program as Condition Report 22781.

Analysis. The failure to submit a timely and complete licensee event report was a

performance deficiency. The inspectors reviewed this issue in accordance with

Inspection Manual Chapter 0612 and the NRC Enforcement Manual. Through this

review, the inspectors determined that traditional enforcement was applicable to this

issue because the NRC's regulatory ability was affected. Specifically, the NRC relies on

the licensee to identify and report conditions or events meeting the criteria specified in

regulations in order to perform its regulatory function, and when this is not done, the

regulatory function is impacted. The inspectors determined that this finding was not

suitable for evaluation using the significance determination process, and as such, was

evaluated in accordance with the NRC Enforcement Policy. The finding was reviewed

by NRC management, and because the violation was determined to be of very low

safety significance, was not repetitive or willful, and was entered into the corrective

action program, this violation is being treated as a Severity Level IV noncited violation

consistent with the NRC Enforcement Policy. This finding was determined to have a

crosscutting aspect in the area of problem identification and resolution associated with

the corrective action program in that the licensee failed to appropriately and thoroughly

evaluate for reportability aspects all factors and time frames associated with the

inoperability of the engineered safety features actuation system P.1(c).

Enforcement. Title 10 CFR 50.73(a)(1) requires, in part, that licensees shall submit a

licensee event report for any event of the type described in this paragraph within 60

days after the discovery of the event. Title 10 CFR 50.73(a)(2)(v) requires, in part, that

events or conditions that could have prevented the fulfillment of the safety function of

structures or systems that are needed to shutdown the reactor and maintain it in a safe

shutdown condition, remove residual heat, control the release of radioactive material, or

mitigate the consequences of an accident. Contrary to the above, on October 23, 2009,

Wolf Creek failed to submit a licensee event report within 60 days for removing the P-4

interlock from service, and failed to identify that the condition could have prevented the

fulfillment of the safety function of structures or systems that are needed to mitigate the

consequences of an accident. In accordance with the NRC's Enforcement Policy, the

finding was reviewed by NRC management and because the violation was of very low

safety significance, was not repetitive or willful, and was entered into the corrective

action program, this violation is being treated as a Severity Level IV noncited violation,

consistent with the NRC Enforcement Policy: NCV 05000482/2009005-15, Failure to

Report a Condition that Could Have Prevented Fulfillment of a Safety Function.

4OA5 Other Activities

.1

Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope

During the inspection period, the inspectors performed observations of security force

personnel and activities to ensure that the activities were consistent with Wolf Creek

- 69 -

Enclosure 2

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status review and inspection activities.

b.

Findings

No findings of significance were identified.

.2

Temporary Instruction 2515-172, Reactor Coolant System Dissimilar Metal Butt Welds

a.

Inspection Scope:

Portions of Temporary Instruction 2515/172, Reactor Coolant System Dissimilar Metal

Butt Welds, were performed at Wolf Creek during Refueling Outage 17. Specific

documents reviewed during this inspection are listed in the attachment. This unit has

the following dissimilar metal butt welds.

COMPONENT ID

DESCRIPTION

MRP-139

CATEGORY

BASELINE

EXAM

COMMENT

RV-301-121-A

Loop 1 Outlet

Nozzle to Safe-

end weld

D

April 2005

RF14

Next exam:

October 2009

RF17

RV-301-121-B

Loop 2 Outlet

Nozzle to Safe-

end weld

D

April 2005

RF14

Next exam:

October 2009

RF17

RV-301-121-C

Loop 3 Outlet

Nozzle to Safe-

end weld

D

April 2005

RF14

Next exam:

October 2009

RF17

RV-301-121-D

Loop 4 Outlet

Nozzle to Safe-

end weld

D

April 2005

RF14

Next exam:

October 2009

RF17

RV-302-121-A

Loop 1 Inlet

Nozzle to Safe-

end weld

E

April 2005

RF14

Next exam:

April 2011 RF18

RV-302-121-B

Loop 2 Inlet

Nozzle to Safe-

E

April 2005

Next exam:

- 70 -

Enclosure 2

COMPONENT ID

DESCRIPTION

MRP-139

CATEGORY

BASELINE

EXAM

COMMENT

end weld

RF14

April 2011 RF18

RV-302-121-C

Loop 3 Inlet

Nozzle to Safe-

end weld

E

April 2005

RF14

Next exam:

April 2011 RF18

RV-302-121-D

Loop 4 Inlet

Nozzle to Safe-

end weld

E

April 2005

RF14

Next exam:

April 2011 RF18

TBB03-1-W /

MW7090-WOL-DM

Pressurizer surge

nozzle to safe-

end weld

D / F

October 2006

RF15

Note 1

TBB03-2-W /

MW7089-WOL-DM

Pressurizer spray

nozzle to safe-

end weld

D / B

October 2006

RF15

Note 1

TBB03-3-A-W /

MW7086-WOL-DM

Pressurizer

safety nozzle A to

safe-end weld

D / B

October 2006

RF15

Note 1

TBB03-3-B-W /

MW7087-WOL-DM

Pressurizer

safety nozzle B to

Safe-end weld

D / B

October 2006

RF15

Note 1

TBB03-3-C-W /

MW7088-WOL-DM

Pressurizer

safety nozzle C

to safe-end weld

D / F

October 2006

RF15

Note 1

TBB03-4-W /

MW7085-WOL-DM

Pressurizer relief

nozzle to safe-

end weld

D / F

October 2006

RF15

Note 1

Note 1: The pressurizer dissimilar metal butt-welds had full structural weld overlay

applied in Refueling Outage 15. The first Component ID was the designation prior to

overlay, the latter Component ID is the current weld designation (after overlay).

Likewise, the first MRP-139 category was the designation prior to baseline exam and

overlay, and the latter is the current designation (after overlay). Note that these

locations are now examined in accordance with approved alternative of relief

Request I3R-05.

- 71 -

Enclosure 2

03.01 Licensees Implementation of the MRP-139 Baseline Inspections

a.

MRP-139 baseline inspections:

The inspectors reviewed records nondestructive examination activities associated with

the licensees hot leg inspection effort. The baseline inspections of the pressurizer

dissimilar metal butt welds were completed during the spring 2008 Refueling Outage 16.

b.

At the present time, the licensee is not planning to take any deviations from the baseline

inspection requirements of MRP-139, and all other applicable dissimilar metal butt welds

are scheduled in accordance with MRP-139 guidelines.

03.02 Volumetric Examinations

a.

The inspectors reviewed the ultrasonic examination records of the four unmitigated

reactor hot leg nozzles and piping. The inspectors concluded that the ultrasonic

examination for these welds was done in accordance with ASME Code,Section XI,

Supplement VIII, Performance Demonstration Initiative requirements regarding

personnel, procedures, and equipment qualifications. No relevant conditions were

identified during these examinations.

b.

The inspectors reviewed the nondestructive evaluations performed on the four reactor

hot leg nozzles and piping. Inspection coverage met the requirements of MRP-139 and

no relevant conditions were identified.

c.

The certification records of examination personnel were reviewed for those personnel

that performed the examinations of the inspected nozzles. All personnel records

showed that they were qualified under the EPRI Performance Demonstration Initiative.

d.

No deficiencies were identified during the nondestructive evaluations.

03.03 Weld Overlays.

The licensee performed all weld overlays during the previous outage (RF 15).

03.04 Mechanical Stress Improvement

The licensee did not employ a mechanical stress improvement process this outage.

03.05 Inservice inspection program

a.

Inspection Scope:

The licensees MRP-139 program is part of their Alloy 600 program and future

inspections are in accordance with the MRP-139 requirements.

- 72 -

Enclosure 2

b.

Findings

No findings of significance were identified.

.3

(Closed) Unresolved Item 05000482/2008010-04: Operator Actions May Create the

Potential for Secondary Fires

Introduction. The inspectors identified a Green non-cited violation of License

Condition 2.C.(5), Fire Protection, for the failure to implement and maintain the

approved fire protection program. Specifically, the licensee prescribed mitigating actions

in response to certain fire scenarios that would result in a loss of circuit breaker

coordination and could initiate secondary fires in plant locations outside of the initial fire

area.

Description. Procedure OFN KC-016, Fire Response, Revision 19, specified operator

actions to be taken in response to fires outside of the control room. This procedure

provided the mitigating actions needed to maintain the reactor in hot standby in the

event of various failures and spurious actuations. The inspectors identified the following

13 fire areas where the prescribed mitigating actions would remove electrical circuit

protection (i.e., circuit breaker coordination) for the train affected by the fire and could

initiate secondary fires in plant locations outside of the initial fire area:

Fire Area A-8

Auxiliary Building - 2000 Elevation, General Area

Fire Area A-11

Cable Chase (Room 1335)

Fire Area A-16

Auxiliary Building - 2026 Elevation, General Area

Fire Area A-17

South Electrical Penetration (Room 1409)

Fire Area A-18

North Electrical Penetration (Room 1410)

Fire Area C-18

North Vertical Cable Chase (Room 3419)

Fire Area C-21

Lower Cable Spreading (Room 3501)

Fire Area C-22

Upper Cable Spreading (Room 3801)

Fire Area C-23

South Vertical Cable Chase (Room 3505)

Fire Area C-24

North Electrical Chase (Room 3504)

Fire Area C-30

South Vertical Cable Chase (Room 3617)

Fire Area C-33

South Vertical Cable Chase (Room 3804)

Fire Area RB

Reactor Building (Containment)

For these fire areas, the procedure directed the operators to remove power to a

power-operated relief valve if a fire caused the power-operated relief valve to spuriously

open and operators could not close its associated block valve. Specifically, the

procedure directed the operators to open circuit breakers on the associated 125 Vdc

power supply. The inspectors noted that the failure of the block valve to close resulted

from fire damage and not from a spurious operation of the valve.

The licensee specified this action in order to close the power-operated relief valve and

preclude the potential for spurious opening due to inter-cable faults (i.e., cable-to-cable

hot shorts). However, the inspectors determined this action would also remove the

control power used to operate 4160 Vac and 480 Vac circuit breakers. The removal of

- 73 -

Enclosure 2

control power would prevent remote breaker operations and disable the circuit breaker

protective trips for the train affected by the fire.

Removing control power to the circuit breaker results in a loss of its ability to

automatically isolate faults before severe damage occurs. As a result, fire-induced faults

(shorts to ground) in non-essential power cables of the affected 4160 Vac and 480 Vac

supplies may not clear until after tripping an upstream feeder breaker to the supplies,

which would remove power from equipment that was assumed by the safe shutdown

analysis to be unaffected. This action would also prevent breakers from automatically

opening during an overload condition and could initiate secondary fires in plant locations

outside of the initial fire area.

The safe shutdown analysis assumed that a fire occurred in one fire area at any time.

The inspectors determined that the mitigating actions taken in response to fires in the

listed fire areas had the potential to initiate secondary fires in other plant locations, which

would invalidate the safe shutdown analysis and could impact the ability to achieve and

maintain safe shutdown.

Analysis. Prescribing mitigating actions in response to certain fire scenarios that would

result in a loss of circuit breaker coordination and could initiate secondary fires in plant

locations outside of the initial fire area was a performance deficiency. The inspectors

determined that this deficiency was more than minor because it was associated with the

Protection Against External Factors attribute of the Initiating Events Cornerstone and

adversely affected the cornerstone objective to limit the likelihood of those events that

upset plant stability and challenge critical safety functions during shutdown as well as

power operations.

The significance of this finding was evaluated using the Significance Determination

Process in Manual Chapter 0609, Appendix F, Fire Protection Significance

Determination Process, because it affected fire protection defense-in-depth strategies

involving post-fire safe shutdown systems.

The inspectors associated the finding with the post-fire safe shutdown category since the

performance deficiency would remove power from equipment that was assumed by the

safe shutdown analysis to be unaffected and could initiate secondary fires in plant

locations outside of the initial fire area. The inspectors assigned the finding a high

degradation rating since the affected circuit breakers would not provide any fire

protection benefit and would receive no fire protection credit.

The inspectors performed a Phase 2 evaluation to determine an upper limit for the

change in core damage frequency. The inspectors determined eight credible fire

scenarios that could result in core damage under certain conservative assumptions. The

pertinent parameters and results of these scenarios are summarized below.

Attachment B provides a more detailed discussion of the Phase 2 evaluation.

- 74 -

Enclosure 2

Table 1. Phase 2 Evaluation Results

Scenario

Number

Ignition

Source

Source

Description

(Fire Area)

Fire

Ignition

Frequency

Heat

Release

Rate

Severity

Factor

Probability of

Non-Suppression

Probability

of a Hot

Short

CCDP

1

RP-333

Relay

Panel

(A-16)

6.00E-5

200 kW

0.9

0.35

0.02

3.78E-7

2

RP-333

Relay

Panel

(A-16)

6.00E-5

650 kW

0.1

0.35

0.02

4.20E-8

3

SK194B

Security

Panel

(A-16)

6.00E-5

200 kW

0.1

0.35

0.02

4.20E-8

4

NG01B

600V MCC

(A-18)

6.00E-5

200 kW

0.1

0.44

0.02

5.28E-8

5

Transient

Fire

C-21

6.26E-6

70 kW

0.9

0.26

0.02

2.93E-8

6

Transient

Fire

C-21

6.26E-6

200 kW

0.1

0.26

0.02

3.26E-9

7

Transient

Fire

C-22

5.54E-6

70 kW

0.9

1.00

0.02

9.96E-8

8

Transient

Fire

C-22

5.54E-6

200 kW

0.1

1.00

0.02

1.11E-8

Total

6.58E-7

In each of these scenarios, the conditional core damage probability (CCDP) bounds the

change in core damage frequency. The inspectors calculated the conditional core

damage probability using the following equation:

Short

Hot

n

Suppressio

Non

P

x

P

x

SF

x

FIF

CCDP

=

where:

FIF denotes the fire ignition frequency

SF denotes the severity factor

n

Suppressio

Non

P

denotes the non-suppression probability

- 75 -

Enclosure 2

Short

Hot

P

denotes the probability of a hot short

The sum of the conditional core damage probabilities for each of the fire scenarios

bounded the total change in core damage frequency associated with this performance

deficiency. Since the change in core damage frequency exceeded1E-7, the inspectors

screened the finding for its potential risk contribution to a large early release frequency.

In accordance with the guidance in NRC Inspection Manual Chapter 0609, Appendix H,

the inspectors determined this finding did not involve a significant increase in the risk of

a large early release of radiation because Wolf Creek has a large, dry containment and

the accident sequences contributing to a change in the core damage frequency did not

involve either a steam generator tube rupture or an intersystem loss of coolant accident.

Since this bounding change in core damage frequency was less than 1E-6/year and the

finding did not involve a significant increase in the risk of a large early release frequency,

the inspectors determined this performance deficiency had very low risk significance

(Green). This finding was not assigned a cross-cutting aspect because it existed more

than two years and does not represent current performance.

As a compensatory measure, the licensee implemented an hourly fire watch in the

affected fire areas, with the exception of the reactor building, which is not readily

accessible during power operations. For the reactor building, the licensee is monitoring

the containment temperature as a compensatory measure.

Enforcement. License Condition 2.C.(5) states, in part, that the licensee shall maintain

in effect all provisions of the approved fire protection program as described in the

Standardized Nuclear Unit Power Plant System (SNUPPS) Final Safety Analysis Report

for the facility through Revision 17, the Wolf Creek Site Addendum through Revision 15,

and as approved in the Safety Evaluation Report through Supplement 5. The Wolf

Creek Updated Safety Analysis Report combined the SNUPPS Final Safety Analysis

Report, Revision 17, and the Wolf Creek Site Addendum, Revision 15, into one

document.

Appendix 9.5B of the Updated Safety Analysis Report provides an area-by-area analysis

of the power block that incorporated Drawing E-1F9905, Fire Hazards Analysis,

Revision 2, by reference. Drawing E-1F9905 states that the overall intent is to

demonstrate that a single plant fire will not negatively affect the post-fire safe shutdown

capability and that if a circuit damaged by a fire is protected by an individual overcurrent

protection device, that device is assumed to function to clear the fault.

Contrary to the above, prior to December 22, 2009, the licensee failed to implement and

maintain in effect all provisions of the approved fire protection program. Specifically, the

licensee prescribed mitigating actions in response to certain fire scenarios that would

result in a loss of circuit breaker coordination (i.e., disable an overcurrent protection

device from functioning to clear a fault) and could initiate secondary fires in plant

locations outside of the initial fire area that negatively affect the post-fire safe shutdown

capability. However, the plants post-fire safe shutdown capability only evaluated

damage resulting from a single fire.

- 76 -

Enclosure 2

The licensee entered this issue into their corrective action program as Performance

Improvement Request 2008-005210. Because this violation was of very low safety

significance and it was entered into the corrective action program, this violation is being

treated as a non-cited violation, consistent with the NRC Enforcement Policy:

NCV 05000482/2009005-16, Operator Actions Disable Circuit Breaker Coordination and

Could Initiate Secondary Fires.

.4

(Closed) Unresolved Item 05000482/2008010-01: Post-fire Safe Shutdown Inspection

Did Not Identify Diagnostic Information

During a triennial fire protection inspection in 2008, the inspectors identified an

unresolved item concerning the availability of diagnostic instrumentation needed to

respond to a loss of reactor coolant pump seal cooling during certain fire scenarios. The

plant design uses reactor coolant pump seal injection and thermal barrier cooling to cool

the reactor coolant pump seals. One method of seal cooling must be maintained during

reactor coolant pump operation to prevent seal failure, which, in some cases, could lead

to increased seal leakage beyond the capacity of the charging pump.

The licensee identified that fire damage in four fire areas could isolate both methods of

seal cooling. The inspectors identified that the licensee relied upon a decrease in

pressurizer level to diagnose a loss of seal cooling. The inspectors determined the fire

response procedure was inadequate since pressurizer level would not decrease until

after seal failure occurred. Since the procedure required operators to recognize the loss

of cooling and take response actions and the procedure did not identify adequate

instrumentation to be used, the inspectors could not verify that it would remain free of

fire damage for fires in these four fire areas.

In response to the unresolved item, the licensee determined the instrumentation that

would be available to diagnose a loss of seal cooling for fires in these four areas. The

licensee determined that the thermal barrier flow switches and alarms would remain

available for all four areas. The licensee also determined that seal injection flow and

temperature would remain available for most, if not all, of the trains for each fire area.

The inspectors reviewed the abnormal operating procedures used in the event of reactor

coolant pump problems. Based on this review and the licensees analysis of available

instrumentation, the inspectors concluded that it was reasonable to believe that

operators had sufficient instrumentation and guidance to promptly recognize, diagnose,

and respond to a loss of reactor coolant pump seal cooling.

The failure to establish written procedures adequately implementing the approved fire

protection program was a performance deficiency and a violation of Technical

Specification 5.4.1.d. The inspectors determined this performance deficiency was of

minor safety significance since it was not similar to any example in Manual

Chapter 0612, Appendix E, nor did it meet any of the minor questions in Manual

Chapter 0612, Appendix B. This performance deficiency constitutes a violation of minor

significance that is not subject to enforcement action in accordance with the NRCs

Enforcement Policy.

- 77 -

Enclosure 2

The licensee implemented an hourly fire watch as an immediate compensatory measure

and entered this issue into their corrective action program as Condition

Report 2008-005171.

.5

(Closed) Licensee Event Report 05000482/2008006-00: Entry Into Mode 4 Without An

Operable Containment Spray System

On July 3, 2008, Wolf Creek submitted LER 2008006 which described missed VT-2 weld

inspections when modifying train B containment spray recirculation line in refueling

outage 16. Wolf Creek stated that changes to shim the recirculation line inadvertently

resulted in missing the VT-2 post-maintenance test. This resulted in ascending to Mode

4 without an operable containment spray system. Wolf Creek identified this issue on

May 8, 2008, at 1:45am and entered Technical Specification 3.6.6 while in Mode 4. The

VT-2 inspections were performed satisfactorily and Technical Specification 3.6.6 was

exited at 3:13am on May 8, 2008. Enforcement aspects are discussed in Section 4OA7.

This LER is closed.

.6

(Closed) Licensee Event Report 05000482/2008-08-00, -01, -02: Potential for Residual

Heat Removal Trains to be Inoperable during Mode Change.

All three revisions of this licensee event report were discussed and enforcement action

was taken in NRC Inspection Report 05000482/2009006. This licensee event report is

closed.

.7

(Closed) Unresolved Item 2008005-02: Residual Heat Removal Suction Piping

Saturation Temperature and Pressure.

This unresolved item was inspected and enforcement action was taken in NRC

Inspection Report 05000482/2009006. This unresolved item is closed.

.8

(Closed) Licensee Event Report 05000482/2008-004-01: Loss of Power Event When

the Reactor was Defueled.

Licensee Event Report 05000482/2008-004-00 was closed in NRC Inspection

Report 05000482/2008004 as a Green finding. In NRC Inspection

Report 05000482/2009004, the inspectors identified a violation of 10 CFR 50.73

associated with this event report. Wolf Creek subsequently submitted revised Licensee

Event Report 2008-004-01 in response to the Severity Level IV violation. The submittal

of Licensee Event Report 05000482/2008-004-01 restores compliance with

10 CFR 50.73. This licensee event report is closed.

4OA6 Meetings

Exit Meeting Summary

On October 22, 2009, the radiation protection inspectors presented the inspection results

to Mr. M. W. Sunseri and other members of the licensee staff. The licensee

- 78 -

Enclosure 2

acknowledged the issues presented. The inspector asked the licensee whether any

materials examined during the inspection should be considered proprietary. No

proprietary information was identified.

On October 30, 2009, the in-service inspection inspectors debriefed the inspection

results to Mr. M. W. Sunseri, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspectors acknowledged review of proprietary

material during the inspection which had been or will be returned to the licensee.

On December 17 and 22, the fire protection inspectors conducted telephonic exit

meetings and presented the results of the staffs closure of fire protection unresolved

items. The inspectors presented the results to L. Ratzlaff, Manager Support

Engineering, on December 17 and M.W. Sunseri, on December 22. The licensee

acknowledged the issues presented. The inspectors asked the licensee whether any of

the material examined during the inspection should be considered proprietary. No

proprietary information was identified.

On January 14, 2010, the resident inspectors presented the inspection results of the

resident inspections to Mr. M.W. Sunseri, and other members of the licensee's

management staff. The licensee acknowledged the findings presented. The inspectors

noted that while proprietary information was reviewed, none would be included in this

report.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as noncited violations.

.1

On October 22, 2009, at 12:06 p.m., the Wolf Creek control room received trouble

annunciators for emergency diesel generator A. Emergency diesel generator B was out

of service for planned maintenance. 10 CFR 50.47(b)(4) requires that a standard

emergency classification action level scheme be used by the licensee. Wolf Creek

EAL 6, Loss of Electrical Power/Assessment Capability, requires, in part, that when

both emergency diesel generators are out of service for greater than 15 minutes, a

Notice of Unusual Event be declared. Contrary to the above, on October 22, 2009, Wolf

Creek did not declare a Notice of Unusual Event until 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after both emergency

diesel generators were out of service. This issue is of very low safety significance

(Green) because it is associated with failure to report a Notification of Unusual Event.

Wolf Creek initiated Condition Report 21058 regarding the late declaration.

.2

On July 3, 2008, Wolf Creek submitted Licensee Event Report LER 2008006 which

described missed VT-2 weld inspections when modifying train B containment spray

recirculation line in Refueling Outage 16, requiring the train to be declared inoperable.

This issue has been entered in to the corrective action program as Condition

Report 2008-2197. Technical Specification 3.0.4, states, in part, that when a limiting

condition of operation is not met, that mode changes shall only be made: when actions

to be entered permit continued operation for an unlimited period of time, after a risk

- 79 -

Enclosure 2

assessment, or when an allowance is stated in the specification. Technical Specification

Limiting Condition of Operation 3.6.6 requires, in part, two operable trains of

containment spray in Modes 1 through 4. Contrary to the above, on May 8, 2008, Wolf

Creek entered Mode 4 with only one operable containment spray system. This issue is

of very low safety significance (Green) because there was no loss of function of the

containment spray system.

A-1

Attachment 1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

R. D. Benham, Integrated Plant Scheduling

T. D. Card, Engineering

B. E. Dale, Manager Maintenance

T. M. Damashek, Superintendent, Operations Support

T. F. East, Manager, Emergency Planning

D. L. Fehr, Manager Information Systems

R. L. Gardner, Manager, Quality

S. E. Hedges, Vice President Oversight

D. M Hooper, Supervisor Licensing

J. K. Kent, Finance Management

W. R. Ketchum, Supervisor, Plant Safety Assessment

S. R. Koenig, Corrective Actions

W. T. Muilenburg, Licensing

P. J. Bedgood, Superintendent, Chemistry/Radiation Protection

C. L. Palmer, Major Modifications

J. M. Pankaskie, Supervisor, Design Engineering

E. M. Peterson, Ombudsman

D. Phelps, Owners Representative

B. Poteat, Piedmont

L. Ratzlaff, Manager, Support Engineering

E. A. Ray, Manager Chemistry/Health Physics

K. Scherich, Director Engineering

A. F. Stull, Vice President & Chief Administrative Officer

M. W. Sunseri, President and Chief Executive Officer

B. J. Vickery, Supply Chain

B. Walters, Supervisor, Security

M. J. Westman, Manager, Training

K. Frederickson, Licensing

J. Suter, Fire Protection

NRC Personnel

D. Loveless, Senior Reactor Analyst

A-2

Attachment 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed 05000482/2009005-02

NCV

Control of Transient Ignition Sources (Section 1R05)05000482/2009005-03

NCV

Failure to Identify Sources of Boron Leakage

(Section 1R08)05000482/2009005-04

NCV

Failure to Incorporate Requirements of Regulatory

Guide 1.182 into Daily Shutdown Risk Assessment

(Section 1R13.1)05000482/2009005-05

NCV

Mode Change Under Technical Specification 3.0.4.b

Without Required Risk Management Actions

(Section 1R13.2)05000482/2009005-06

NCV

Failure to Follow Corrective Action Procedure

(Section 1R13.3)05000482/2009005-07

NCV

Failure to Follow Procedure Results in Draining of

Emergency Core Cooling System Pump Oil

(Section 1R13.4)05000482/2009005-08

NCV

Inadequate Operability Evaluation of Essential Service

Water Pumps (Section 1R15.1)05000482/2009005-09

NCV

Positive Reactivity Addition Prohibited by Technical

Specifications while in Mode 2 (Section 1R15.2)05000482/2009005-10

NCV

Failure to Obtain Vendor Data Necessary for Plant

Modification (Section 1R18)05000482/2009005-12

NCV

Unevaluated Scaffold Against Component Cooling Water

Piping (Section 1R20)05000482/2009005-13

NCV

Failure to Maintain Administrative Control of Keys to

Locked High Radiation Areas (Section 2SO1)05000482/2009005-14

NCV

Failure to Identify Inoperable P-6 Interlock and

Intermediate Range Detector (Section 4OA2)05000482/2009005-15

NCV

Failure to Report a Condition that Could Have Prevented

Fulfillment of a Safety Function (Section 4OA3)05000482/2009005-16

NCV

Operator Actions disable Circuit Breaker Coordination and

Could Initiate Secondary Fires (Section 4OA5.1)

A-3

Attachment 1

Opened 05000482/2009005-01

VIO

Failure to Correct Discolored Boric Acid Deposits

(Section 1R05)05000482/2009005-11

VIO

Failure to Correct Vessel Head Vent Path (Section 1R20)

Discussed 05000482/2009002-07

VIO

Failure to correct component cooling water valve closures

(EA-09-110) (Section 1R18)

05000482/2009-005-00

LER

Loss of both Diesel Generators with all fuel in the Spent

Fuel Pool (Section 4OA3)

Closed 05000482/2008010-01

URI

Post Fire Safe Shutdown Procedure Did Not Identify

Diagnostic Information (Section 4OA5.4)05000482/2008010-04

URI

Operator Actions May Create the Potential for Secondary

Fires (Section 4OA5.3)

05000482/2008-006-00

LER

Entry Into Mode 4 Without An Operable Containment

Spray System (4OA5.5)

05000482/2008-008-00

05000482/2008-008-01

05000482/2008-008-02

LER

Potential for Residual Heat Removal Trains to be

Inoperable during Mode Change (Section 4OA5.6)05000482/2008005-02

URI

Residual Heat Removal Suction Piping Saturation

Temperature and Pressure (Section 4OA5.7)

05000482/2008-004-01

LER

Loss of Power Event When the Reactor was Defueled

(Section 4OA5.8)

LIST OF DOCUMENTS REVIEWED

Section 1RO1: Adverse Weather Protection

MISCELLANEOUS

NUMBER

TITLE

REVISION

FL-01

Flooding of Auxiliary Building

01

CR 22801

Auxiliary Building Flooding Question

3.4.1

Updated Safety Analysis Report, Flood Protection

19

A-4

Attachment 1

Section 1RO4: Equipment Alignment

PROCEDURES

NUMBER

TITLE

REVISION

M-12EC01

Fuel Pool Cooling and Clean-up System

19

SYS EC-120

Fuel Pool Cooling and Clean-up System Startup

44

CKL EC-120

Fuel Pool Cooling and Clean-up System Normal

Valve Lineup/Breaker Checklist

14A

CKL JE-120

Emergency Fuel Oil System Lineup

19

STS NB-005

Breaker Alignment Verification

18

CKL KJ-121

Diesel Generator NE01 and NE02 Valve Checklist

28A

FPPM-015

Fuel Building Elevation 2000

7

Section 1RO5: Fire Protection

PROCEDURES

NUMBER

TITLE

REVISION

FPPM-009

Control Bldg El. 2000

2

AP 10-106

Fire Preplans

7

Fppm-015

Fuel Building Elevation 2000

7

Section 1RO6: Flood Protection Measures

MISCELLANEOUS

NUMBER

TITLE

ALR 00-095C

AFP Sump Room Level Hi

FL-14

Feed Pump Room Maximum Flood Level

LE-M-002

Auxiliary Building Room 1206, 1207 Maximum Flood

Level

WORK ORDER

WO 08-304475-000

A-5

Attachment 1

Section 1RO7: Heat Sink Performance

PROCEDURES

NUMBER

TITLE

REVISION

STN PE-038

Containment Cooler Performance Test

10

EPRI NP-7552

Heat Exchanger Performance Monitoring Guidelines

1991

Section 1RO8: Inservice Inspection Activities

CONDITION REPORTS

00003599

00011297

00011954

00018217

00018785

00019248

00020993

00021274

2008-004840

CONDITION REPORT GENERATED FOR THIS INSPECTION

00020993, Fire Watches

DRAWINGS

NUMBER

TITLE

REVISION

E 11173-171-005

Westinghouse Electric corporation General Arrangement

Plan

001

E 11373-101-005

Westinghouse Electric Corporation Closure Head

Assembly

002

E 1455E85,

Sheet 1

Westinghouse Electric Corporation Closure Head (SAP)

General Assembly

001

E 6467E69

Wolf Creek Simplified Head Assembly Radiation Shield

Assembly

006

M 164-00043

Mirror Insulation

W008

M-189-50EJ-02-04

Residual Heat Removal B Train RHR Pump Suction

00

PROCEDURES

NUMBER

TITLE

REVISION

AI 16F-001

Evaluation of Boric Acid Leakage

5

AI 16F-002

Boric Acid Leakage Management

5

AP 16F-001

Boric Acid Corrosion Control Program

5

A-6

Attachment 1

NUMBER

TITLE

REVISION

29A-003

Steam Generator Management

AP-10-100

Fire Protection Program

14

AP-10-101

Control of Transient Ignition Sources

12

AP-10-102

Control of Combustible Materials

13

AP-21I-001

Temporary Modification

8

APF 28D-001

Self-Assessment Process

11

PDI-ISI-254-SE-

NB

Remote Inservice Examination of Reactor Vessel

Nozzle to Safe End, Nozzle to Pipe, and Safe end to

Pipe Welds Using the Nozzle Scanner

1

PDI-UT-1

PDI Generic Inspection Procedure for the Ultrasonic

Examination of Ferritic Pipe Welds

D

PDI-UT-2

PDI Generic Inspection Procedure for the Ultrasonic

Examination of Austenitic Pipe Welds

C

PDI-UT-6

PDI Generic Inspection Procedure for the Ultrasonic

Examination of Reactor Pressure Vessel Welds

F

QCP-20-501

PT

8

QCP-20-502

MT

8

QCP-20-503

UT Thickness-Wall Thin

3

QCP-20-504

UT For Flaw Detection

5

QCP-20-508

RT Welds and Components

4

QCP-20-510

Ultrasonic Instrument Linearity Verification

3

QCP-20-511

RT of AWS Groove Welds

1B

QCP-20-514

ET Testing

5B

QCP-20-516

PT/NON-STD Temp

05

QCP-20-517

RT Wall Thinning

2A

QCP-20-521

UT Profile and Plotting

1B

QCP-20-522

Ultrasonic Examination of Ferritic Piping Welds

1B

QCP-20-523

Ultrasonic Examination of Austenitic Piping Welds

1B

QCP-20-527

UT- Soldering

1

QCP-20-540

VT-1 Exam

0B

QCP-20-541

VT-3 Exam

2

QCP-20-543

Fluorescent Dye PT Exam

1

A-7

Attachment 1

NUMBER

TITLE

REVISION

SG-CDME-08-15

Wolf Creek RF16 Condition Monitoring Assessment and

Operational Assessment, April 2008

1

SG-SGMP-09-9

Steam Generator Degradation Assessment for Wolf

Creek, RF17 Refueling Outage, October 2009

0

STN PE-040D

RCS Pressure Boundary Integrity Walkdown

3

STN PE-040G

Transient Event Walkdown

0

STS PE-040E

RPV Head Visual Inspection

2

UT-95

Ultrasonic Examination of Austenitic Piping Welds

3

WCRE-18

Boric Acid Corrosion Control Program Plan

1

WORK ORDERS

08-304695-000

09-313385-000

09-320908-000

09-320918-000

08-310117-000

09-318982-001

09-320910-000

09-320918-001

08-310119-000

09-319416-002

09-320910-001

09-320919-000

08-310136-000

09-320490-000

09-320911-000

09-321389-000

08-311159-000

09-320505-000

09-320912-000

08-311161-000

09-320891-000

09-320913-000

WORK REQUESTS

09-076556

09-076676

09-076711

09-076707

09-076561

09-076307

09-076705

09-076712

09-076710

09-076706

MISCELLANEOUS

NUMBER

TITLE

REVISION / DATE

Steam Generator data Analysis Desktop

Instruction

4

SGAMP Self Assessment, Steam Generator Asset

Management Program

October 17, 2008

Boric Acid Corrosion Control Program 2009 3rd

Quarter Inspection/Monitoring Report

October 13, 2009

A-8

Attachment 1

NUMBER

TITLE

REVISION / DATE

Boric Acid Leakage Screening/Evaluation for

Component EMHV8888

October 8, 2008

Boric Acid Leakage Screening/Evaluation for

Component BGHCV0182

January 5, 2009

Boric Acid Leakage Screening/Evaluation for

Component EP8956C

October 19, 2009

Boric Acid Leakage Screening/Evaluation for

Component EMHV8924

October 20, 2009

Boric Acid Leakage Screening/Evaluation for

Component BBPV8702A

October 14, 2009

Boric Acid Leakage Screening/Evaluation for

Component BGHCV0128

July 9, 2009

Boric Acid Leakage Screening/Evaluation for

Component EMV0175

April 8, 2009

Boric Acid Leakage Screening/Evaluation for

Component BBC5413

April 7, 2009

Boric Acid Leakage Screening/Evaluation for

Component HETCV0250

January 13, 2009

Boric Acid Leakage Screening/Evaluation for

Component ECV0048

January 13, 2009

Boric Acid Leakage Screening/Evaluation for

Component ECV0157

January 12, 2009

Boric Acid Leakage Screening/Evaluation for

Component BBHV8351B

January 12, 2009

Boric Acid Leakage Screening/Evaluation for

Component EJ8730A

January 12, 2009

Boric Acid Leakage Screening/Evaluation for

Component EJV0128

January 12, 2009

Boric Acid Leakage Screening/Evaluation for

Component EJFE0619

January 12, 2009

Boric Acid Leakage Screening/Evaluation for

Component BG8405A

January 9, 2009

Boric Acid Leakage Screening/Evaluation for

Component ENV0115

January 9, 2009

Boric Acid Leakage Screening/Evaluation for

Component BGV0526

January 8, 2009

A-9

Attachment 1

NUMBER

TITLE

REVISION / DATE

Boric Acid Leakage Screening/Evaluation for

Component BBV0357

January 5, 2009

Boric Acid Leakage Screening/Evaluation for

Component BGFCV0110A

January 59, 2009

Boric Acid Leakage Screening/Evaluation for

Component BBV0007

October 15, 2009

Ultrasonic Instrument Calibration Data Record and

Certification for Panametrics, Epoch 4,

SN 081574401

September 2, 2009

Transducer Certification for Krautkramer, 113-222-

591, SN 00V0JM

April 26, 2002

Transducer Certification for Krautkramer, 113-222-

591, SN 00V49N

May 16, 2002

Thermometer Certification for PTC, 312F,

SNs 265095, 265109, 265113

January 6, 2009

Krautkramer Transducer Certification, 113-224-

5591, SN SC0123

January 11, 2008

Krautkramer Transducer Certificate of Conformity,

113-234-591, SN SD0172

December 3, 2007

Ultrasonic Instrument Calibration Data Record and

Certification for Krautkramer, USN 60 SW, SN

01R5NW

August 24, 2009

APF 28D-001-02

Self Assessment Report SEL 04-038 , Steam

Generator Program

4

APF-10-102-01

Transient Combustible Materials Permit

3

AWJ003

Ultrasonic Calibration/Examination Sheet for RPV

Meridonal Weld, ISI Number CH-101-104-C

October 22, 2009

AWJ004

Ultrasonic Calibration/Examination Sheet for RPV

Meridonal Weld, ISI Number CH-101-104-B

October 22, 2009

ET 05-0014

Docket 50-482: 10 CFR 50.55a Request Number

I3R-03 for the Third Ten-Year Interval Inservice

Inspection (ISI) Program - Request for Relief to

Allow Use of Alternate Requirements for Snubber

Inspection and Testing

September 28, 2005

ET 06-0010

Docket 50-482: Inservice Inspection Program Plan

for the Third Ten-Year Interval and 10 CFR 50.55a

Requests I3R-01, I3R-02, and I3R-04

March 2, 2006

A-10

Attachment 1

NUMBER

TITLE

REVISION / DATE

ET 06-0021

Docket No. 50-482: 10 CFR 50.55a Request I3R-

05, Installation and Examination of Full Structural

Weld Overlays for Repairing/Mitigating Pressurizer

Nozzle-to-Safe End Dissimilar Metal Welds and

Adjacent Safe End-to-Piping Stainless Steel Welds

May 19. 2006

ET 06-0042

Docket 50-482: Wolf Creek Nuclear Operating

Corporations Response to the September 20,

2006 NRC Request for Additional Information

Regarding 10 CFR 50.55a Request I3R-05

September 27, 2006

ET 06-0043

Docket 50-482: Wolf Creek Nuclear Operating

Corporations Response to NRC Request for

Additional Information Regarding 10 CFR 50.55a

Request I3R-01

October 5, 2006

ET 06-0044

Docket 50-482: Wolf Creek Nuclear Operating

Corporations Revised Commitment Regarding 10

CFR 50.55a Request I3R-05

October 2, 2006

ET 06-0058

Docket No. 50-482: Wolf Creek Nuclear Operating

Corporations Response to the Second NRC

Request for Additional Information Regarding 10

CFR 50.55a Request I3R-01

December 20, 2006

ET 08-0044

Docket No. 50-482: 10 CFR 50.55a Request I3R-

06, Alternative to Examination Requirements of

ASME Section XI for Class 1 Piping Welds

Examined from the Inside of the Reactor Vessel

September 16, 2008

ET 09-0016

Docket No. 50-482: Revision to Technical

Specifications 5.5.9, Steam Generator (SG)

Program, and TS 5.6.10, Steam Generator Tube

Inspection Report, for a Permanent Alternate

Repair Criterion

June 2. 2009

ET 09-0021

Docket No. 50-482: Response to Request for

Additional Information Related to License

Amendment Request for a Permanent Alternate

Repair Criterion to Technical Specification 5.5.9,

Steam Generator (SG) Program

August 25, 2009

ET 09-0023

Docket No. 50-482: Response to Request for

Additional Information Related to License

Amendment Request for a Permanent Alternate

Repair Criterion to Technical Specification 5.5.9,

Steam Generator (SG) Program

September 3, 2009

A-11

Attachment 1

NUMBER

TITLE

REVISION / DATE

ET 09-0024

Docket No. 50-482: Response to Request for

Clarifications in Response to Application for

Withholding Proprietary Information from Public

Disclosure (TAC NO. ME1393)

September 3, 2009

ET 09-0025

Docket No. 50-482: Revision to Technical

Specification (TS) 5.5.9, Steam Generator (SG)

Program, and TS 5.6.10, Steam Generator Tube

Inspection Report

September 15, 2009

I-ENG-023

Steam Generator Data Analysis Guidelines

8

JEW014

Ultrasonic Calibration/Examination Sheet for RHR

Pipe to Pipe Weld , ISI Number EJ-04-F019

October 22, 2009

JEW015

Ultrasonic Calibration/Examination Sheet for

SI/HPCI Pipe to Elbow Weld, ISI Number EM-03-

S015-B

October 22, 2009

M-12KJ04

Piping and Instrumentation Diagram Standby

Diesel Generator B Lube Oil System

13

M-12KJ06

Piping and Instrumentation Diagram Standby

Diesel Generator B Lube Oil System

13

M-13EF08

Piping Isometric Essential Service Water- Diesel

Generator Bldg.

1

QCF 20-510-01

Ultrasonic Instrument Linearity Form

2

QCF-20-100-01

Contractor Certification Review

2

QCF-20-504-02

Ultrasonic Flaw Detection Data Sheet

2

QCF-20-504-06

Ultrasonic Flaw Detection Calibration Data Sheet

0

SAP-+PT-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-+PTUB-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-01-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-02-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-03-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-04-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

A-12

Attachment 1

NUMBER

TITLE

REVISION / DATE

SAP-05-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-06-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-07-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-08-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-09-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-10-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-11-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-12-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-BOB-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-DELTA-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SAP-GHENT-09

Steam Generator Eddy Current Inspection Multi-

Frequency Eddy Current Parameters

0

SEL 04-038

Steam Generator Program

4

SG-CDME-08-15

Wolf Creek RF16 Condition Monitoring

Assessment and Operational Assessment, April

2008

1

SG-CDME-09-1

Wolf Creek Steam Generator Secondary Side

Condition Monitoring and Operational Assessment

for Fuel Cycle and Refueling Outage 17

0

SG-SGMP-09-9

Steam Generator Degradation Assessment for

Wolf Creek, RF17 Refueling Outage, October 2009

0

WDI-LTR-

ENG-09-0016

Technical Justification of the Impact of Using

Tap/Demineralized Water for UT System

Calibration and Borated Reactor Cavity Water for

RVISI UT Examinations.

0

A-13

Attachment 1

Section 1R12: Maintenance Effectiveness

MISCELLANEOUS

NUMBER

TITLE

REVISION /

DATE

EG-01

Maintenance Rule Database - Component Cooling

Water - Engineered Safety Features System Cooling

n/a

EG-03

Maintenance Rule Database - Component Cooling

Water System - RCP Thermal Barrier Cooling

n/a

EG-07

Maintenance Rule Database - Component Cooling

Water System - ESW Frazil Ice Prevention

n/a

M-11EG02

System Flow Diagram Component Cooling Water

System

2

M-762-001-02

Nuclear Instrumentation System Source Range N-31

Functional Block Diagram

7

PIR 2004-1625

Two Source Range Channels are Required to

Perform Core Alterations During a Refueling Outage

June 22,

2004

SE-01

Maintenance Rule Database - Source Range

Nuclear Instrumentation

n/a

SE-02

Maintenance Rule Database - Intermediate Range

Nuclear Instrumentation

n/a

OFN PK-029

Loss of Non-Vital 125 VDC Bus PK01, PK02, PK03,

PK4, and Annunciators

15

STS IC-232

Channel Operational Test Nuclear Instrumentation

System Source Range N-32 Protection Set II

15

AI 28A-023

Evaluation of Maintenance Rule Functional Failure

1

AP 23M-001

WCGS Maintenance Rule Program

7

EDI 23M-050

Establishing Performance Criteria for Structures,

Systems and Components with the Scope of the

Maintenance Rule

3

WCN-7328

Report on ECAD Testing at Wolf Creek Generating

Station

October 28,

2009

WR 5047865

Functional Failure Determination (EDI 23M-050)

April 24,

2005

Maintenance Rule Expert Panel Meeting Minutes

February 18

, 1999

A-14

Attachment 1

NUMBER

TITLE

REVISION /

DATE

Maintenance Rule Expert Panel Meeting Minutes

April 10,

2000

Maintenance Rule Expert Panel Meeting Minutes

April 24,

2000

WORK ORDERS

NUMBER

TITLE

REVISION /

DATE

WO 07-293925-000

Replace Electrolytic Capacitors or Replace Power

Supply NIS Source Range Hi Voltage Power Supply

March 31,

2008

WO 08-302634-000

Perform STN IC-031 Source Range N-31 High Flux

at Shutdown Alarm Calibration

January 12,

2008

WO 08-302635-000

Perform STN IC-032 Source Range N-32 High Flux

at Shutdown Alarm Calibration

January 12,

2008

WO 08-305403-000

Refuel 16 Perform STN IC-031 Source Range N-31

High Flux at Shutdown Alarm Calibration

April 11,

2008

WO 08-305404-000

Refuel 16 Perform STN IC-032 Source Range N-32

High Flux at Shutdown Alarm Calibration

April 11,

2008

WO 08-310573-000

Replace Electrolytic Capacitors or Replace Power

Supply

August 13,

2009

WO 09-314187-000

Retorque CCW Pump to Motor Coupling Bolts

February

12, 2009

WO 09-316487-000

Troubleshoot IR SE NI-36 to Determine Why it Hung

Up Following RX Trip on 4/28 and Repair as

Necessary

April 28,

2009

WO 09-318691-000

Troubleshoot CCW Return from RCP Thermal

Barrier High Flow Setpoint

September

22, 2009

WO 09-320716-000

Refuel 17. Perform Detector and Cable Integrity

Checks for SR, IR, and PR NIS Channels

October 10,

2009

WO 09-320874-000

Troubleshoot Source Range Channel 31 to

Determine Why it Failed After it was Energized

October 10,

2009

WO 09-320874-001

Replace High Voltage Power Supply (NQ101) in

N-31 Source Range during partial STS IC-431

October 10,

2009

WO 09-320874-005

Replace R150 in N-31

October 10,

2009

A-15

Attachment 1

NUMBER

TITLE

REVISION /

DATE

WR 09-076482

During the Performance of STS IC-432 the Two-Phi

Meter Failed to Alarm Annunciator

October 24,

2009

WORK ORDERS

WO 05-270366-000

WO 05-270366-006

WO 06-288260-000

CONDITION REPORTS

CR 20052

CR 01880

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

MISCELLANEOUS

NUMBER

TITLE

REVISION /

DATE

AP 22B-001

Outage Risk Management

11

AP 22C-003

Operational Risk Assessment Program

14A

AP 23M-001

WCGS Maintenance Rule Program

7

APF 22B-001-02

Daily Shutdown Risk Assessments for RFO 17

8

AI-07A-008

Lake Water Chemical Treatment Program

16

AP 23L-001

Lake Water Systems Corrosion and Fouling

Mitigation Program

2

SYS EF-300

ESW/Service Water Macrofoul Treatment

22

WCEM-06-005

Zebra Mussel Monitoring - 2008 Report and 2009

Plan

9

RNT 745679/0

Assessment of the Potential Impact of Zebra

Mussels on the Wolf Creek Power Plant and

Recommendations for Control

July 20, 2009

900030

Customer Assembly Neutron Flux Monitor System,

SNUPPS Generating Stations, Callaway 1 (Union

Elec Co) and Wolf Creek (Kansas Gas & Electric)

F

CCP 013096

Instrument Setpoints for RCP Thermal Barrier

Isolation and EGHV0062 Valves

1

A-16

Attachment 1

NUMBER

TITLE

REVISION /

DATE

EQDP-ESE-47A

Boron Dilution Fix: Source/Intermediate Range

Neutron Detector

0

M-762-00018-W03

Source and Intermediate Range Detector Assembly

August 19,

1988

NY-10042

Class 1E Qualified Proportional Counter and

Compensated Ionization Chamber Insulated

Assembly

September

1990

NY-10044

Qualified* Class 1E BF3 Proportional Counter

Assembly

September

1990

OE SE-09-008

Source Range Nuclear Instrument SEN0031

00

OE SE-09-011

Source Range Nuclear Instrument SEN0032

00

USAR 9.4.6

Containment HVAC

19

STS AE-205

Feedwater System Inservice Valve Test

November 120

09

LCO 3.0.4

Wolf Creek Technical Specifications

November 182

009

APF 22C-003-01

Operational Risk Assessment

November 172

009

n/a

Wolf Creek Operations Logs: Control Room Log

n/a

n/a

Wolf Creek Operations Logs: Equipment Out of

Service Log

n/a

n/a

Technical Specification LCO 3.0.4 Mode Change

Review Form - TDAFWP Inoperable

November 17,

2009

CONDITION REPORTS

NUMBER

TITLE

REVISION /

DATE

CR 19528

SOER 09-1: Shutdown Safety

September 1,

2009

CR 21286

ESW Self Cleaning Strainer Tubes Retain Debris

October 28,

2009

CR 19282

Source Range N31 Indication During Loss of Cavity

Cooling

August 20,

2009

A-17

Attachment 1

NUMBER

TITLE

REVISION /

DATE

CR 20208

Source Range Detector Operability Question

September 30,

2009

CR 20325

Effect on Cavity Components with Loss of Cavity

Cooling

October 6,

2009

CR 21906

T/S Log Entries Related to Entering Mode 3 with

TDAFWP OOS

November 19,

2009

CR 21926

Inconsistent Directions for Protected Train Signs in

Mode 3

November 19,

2009

CR 21286

ESW Self Cleaning Strainer Tubes Retain Debris

October 28,

2009

WORK ORDERS

NUMBER

TITLE

REVISION /

DATE

WO 09-322198-000

Create a RM/Repetitive Task to Open the ESW Self

Cleaning Strainers and Clean the Porous Strainer

Tubes

November 12,

2009

WO 09-319411-001

Source Range NI 31 Indication is Trending Up.

Evaluate Condition to Determine Cause

August 22,

2009

Section 1R15: Operability Evaluations

MISCELLANEOUS

NUMBER

TITLE

REVISION /

DATE

OE SE-09-008

Source Range Nuclear Instrument SEN0031

00

AI-07A-008

Lake Water Chemical Treatment Program

16

AP 23L-001

Lake Water Systems Corrosion and Fouling

Mitigation Program

2

AP 28-001

Operability Evaluations

17

AP 26C-004

Technical Specification Operability

January 13,

2010

SYS EF-300

ESW/Service Water Macrofoul Treatment

22

WCEM-06-005

Zebra Mussel Monitoring - 2008 Report and 2009

Plan

9

A-18

Attachment 1

NUMBER

TITLE

REVISION /

DATE

RNT 745679/0

Assessment of the Potential Impact of Zebra

Mussels on the Wolf Creek Power Plant and

Recommendations for Control

July 20,

2009

900030

Customer Assembly Neutron Flux Monitor System,

SNUPPS Generating Stations, Callaway 1 (Union

Elec Co) and Wolf Creek (Kansas Gas & Electric)

F

CCP 013096

Instrument Setpoints for RCP Thermal Barrier

Isolation and EGHV0062 Valves

1

EQDP-ESE-47A

Boron Dilution Fix: Source/Intermediate Range

Neutron Detector

0

M-762-00018-W03

Source and Intermediate Range Detector Assembly

August 19,

1988

NY-10042

Class 1E Qualified Proportional Counter and

Compensated Ionization Chamber Insulated

Assembly

September

1990

NY-10044

Qualified* Class 1E BF3 Proportional Counter

Assembly

September

1990

OE SE-09-008

Source Range Nuclear Instrument SEN0031

00

OE SE-09-011

Source Range Nuclear Instrument SEN0032

00

USAR 9.4.6

Containment HVAC

19

STS AE-205

Feedwater System Inservice Valve Test

November

9, 2009

n/a

Wolf Creek Operations Logs: Control Room Log

n/a

n/a

Wolf Creek Operations Logs: Equipment Out of

Service Log

n/a

LCO 3.0.4

Wolf Creek Technical Specifications

November

18, 2009

n/a

Technical Specification LCO 3.0.4 Mode Change

Review Form - TDAFWP Inoperable

November

17, 2009

APF 22C-003-01

Operational Risk Assessment

November

17, 2009

M-089-K027-06

Byron Jackson Report DC-1104

3

EF-S-043

Determine the Stress in the Essential Service Water

Pump (PEF01A) column housing using specified

maximum deflection

0

A-19

Attachment 1

CONDITION REPORTS

CR 19282

CR 20208

CR 20325

CR 21906

CR 22798

CR 21574

CR 21400

CR 21572

CR 21926

WORK ORDERS

NUMBER

TITLE

REVISION /

DATE

WO 09-319411-001

Source Range NI 31 Indication is Trending Up.

Evaluate Condition to Determine Cause

August 22,

2009

WO 09-322198-000

Section 1R18: Plant Modifications

NUMBER

TITLE

REVISION

AP 05-010

Design Drawings

6

AP 05D-001

Calculations

12

AP 05A-001

Design Inputs

1

AP 05-002

Dispositions and Change Packages

8

AP 05-005

Design, Implementation & Configuration of

Modifications

13

WCRE-01

Total Plant Setpoint Document

32

CCP 013096

Instrument Setpoints for RCP Thermal Barrier

Isolation and EGHV0062 Valves

01

AP 05-013

Review of Vendor Technical Documents

7A

NP 92-0996

Interoffice Correspondence from C. R. Morris, CCW

Low Transient (PMR 03580) Meeting

5/21/92

EG-M-016

Time Delay for Isolation of CCW High Flow to RCP

Thermal Barriers

1

M-738-0032-02

Functional Requirements and Design Criteria

Standard Single and Twin Units 212, 312, 412 Plants

Component Cooling System

3

CONDITION REPORT

CR 16243

A-20

Attachment 1

Section 1R19: Postmaintenance Testing

NUMBER

TITLE

REVISION

STN EF-201

ESW System Valve Test

2A

AP 16E-002

Post Maintenance Testing Development

8

AP 23D-001

Motor Operated Valve Program

2

STS IC-608A

Slave Relay Test K608A Train A Safety Injection

18

CONDITION REPORT

CR 19670

WORK ORDERS

06-291566-001

06-291566-012

09-316118-001

Section 1R20: Refueling and Other Outage Activities

NUMBER

TITLE

REVISION

WCRE-16

Inservice Inspection Program Plan Wolf Creek

Generating Station Interval 3

4

WCRE-23

Inservice Inspection Classification Basis Document

Wolf Creek Generating Station Interval 3

3/24/09

SYS BB-112

Vacuum Fill of the RCS

27

GEN 00-008

Reduced Inventory Operations

19

GEN 00-009

Refueling

23

GEN 00-003

Hot Standby to Minimum Load

73

SYS BB-215

RCS Drain Down with Fuel in Reactor

23A

STS RE-002

Determination of Estimated Critical Position

18

APF 19C-002-01

Wolf Creek Generating Station Fuel Transfer

Authorization

0

APF 22B-001-02

Daily Shutdown Risk Assessment

8

RWP 092602

Radiation Work Permit

1

RWP 092602

ALARA Review Package

7

RWP 091102

Radiation Work Permit

0

RWP 091102

ALARA Review Package

7

A-21

Attachment 1

NUMBER

TITLE

REVISION

RWP 091102

Radiation Work Permit

0

EID-0003

Refuel Level Indications

2

M-19BG24

Hanger Location DWG. Small Pipe CVCS Auxiliary

Spray Reactor Building

7

M-15BG21

Hanger Location DWG. Small Pipe CVCS - Normal

& Alternate Charging Reactor Building

12

M-12BG01

Piping & Instrumentation Diagram Chemical and

Volume Control System

14

M-12BB02

Piping & Instrumentation Diagram Reactor Coolant

System

16

n/a

Investigation into the Extent of Condition Related to

Linear Indications Discovered on Pressurizer

Auxiliary Spray Line at Wolf Creek Generating

Station

November 4,

2009

CONDITION REPORTS

CR 20528

CR 20628

CR 21366

CR 21387

CR 21719

CR 20622

CR 20893

WORK ORDERS

WO 09-321462-015

WO 08-303356-004

WO 09-321902-001

WO 08-303356-001

Section 1R22: Surveillance Testing

MISCELLANEOUS

NUMBER

TITLE

REVISION

STS AL-210A

MDAFW Pump A inservice check valve test

10

WCOP 02

Inservice Testing Program for Pumps and Valves

14

AP 29B-002

ASME code testing of pumps and valves

7

AP 29B-003

Surveillance Testing

10

AP 29B-001

IST Basis Document

3

A-22

Attachment 1

STS AL-212

MD AFP Comprehensive Pump Testing Flow Path

Verification & Check Valve Testing

14

AP 29A-004

ASME Section XI System Pressure Testing

7

QCP 20-520

Pressure Test Examination

8A

STS PE-007

Periodic Verification of Motor Operated Valves

3

AI 23D-002

MOV Calculation Guidelines

2

AI 23D-003

MOV Trending and Periodic Verification Program

1

AP 29E-001

Program Plan for Containment Leakage

Measurement

12

NEI 94-01

NEI Guideline for Implementing the Performance

Based Guideline of Appendix J

NEI 94-01

M-12AL01

Piping and Instrumentation Drawing Auxiliary

Feedwater

10

M-12AE01

Piping and Instrumentation Drawing Feedwater

37

M-12EF01

Piping and Instrumentation Drawing Essential

Service Water

21

M-12EF02

Piping and Instrumentation Drawing Essential

Service Water

25

M-724-00784

EJHV8811A/B Pressure Locking Bypass

W02

M-724-00696

Motor Operated Gate Valve

W06

M-12EJ01

Piping and Instrumentation Drawing Residual Heat

Removal System

43

CONDITION REPORTS

CR 1994-0881

CR 1998-0422

CR 2001-2237

CR 2005-1899

CR 2005-3545

CR 20723

CR 21308

CR 21343

WORK ORDERS

WO 05-278104-012

WO 09-321637-000

WO 09-321637-002

WO 09-321637-001

A-23

Attachment 1

Section 2OS1: Access Controls to Radiologically Significant Areas

CORRECTIVE ACTION DOCUMENTS

20878

15485

14874

19405

19409

21004

20973

20987

10196

9627

2008-1576

21029

20976

5633

PROCEDURES

NUMBER

TITLE

REVISION

AP 25A-700

Use of Temporary Shielding or Locked High Radiation Areas

and Very High Radiation Area Barricades

10

RPP 02-105

RWP

33

AP 22-01

Conduct of Pre-Job and Post-Job Briefs

9A

AP 25A-200

Access to Locked High or Very High Radiation Areas

20

SEC 01-206

High Security Key Control and Issue

32

AP 25B-200

Radiography Guidelines

12

RADIATION WORK PERMITS

93021

9220

92602

93230

Section 4OA2: Identification and Resolution of Problems

MISCELLANEOUS

NUMBER

TITLE

REVISION

SYS AF-200

High Pressure Heater Operations

8

AP 21-001

Conduct of Operations

43

AP 19E-002

Reactivity Management Program

13

CONDITION REPORTS

CR 18034

CR 04293

CR 2001-2255

A-24

Attachment 1

Section 40A5: Other Activities (TI-172 Dissimilar Metal Welds)

MISCELLANEOUS

NUMBER

TITLE

REVISION

UT-95

Ultrasonic Examination of Austenitic Piping Welds

3

WCRE-24

WESDYNE Year 2009 Reactor Vessel Nozzle Safe-

end Examinations Program Plan

0

WDI-CAL-102

Calibration Inspection Procedure for PCI Eddy

Current Card

1

WDI-EQPT-1021

Installation and Removal of the WESDYNE Nozzle

Scanner (SQUID)

4

WDI-EQPT-1022

Reactor Vessel Nozzle Scanner Setup and Checkout

2

WDI-STD-146

ET Examination of Reactor Vessel Pipe Welds Inside

Surface

9

A2-1

Attachment 2

Attachment 2

Significance Determination Process for Noncited Violation 2009005-16: Operator Actions

Disable Circuit Breaker Coordination and Could Initiate Secondary Fires

Introduction

This attachment discusses the risk significance of Noncited Violation 2009005-16. This

document discusses the methods, assumptions, and results of the significance determination

process.

Methods

The significance of this finding was evaluated using the significance determination process in

Manual Chapter 0609, Appendix F, Fire Protection Significance Determination Process,

because it affected fire protection defense-in-depth strategies involving post-fire safe shutdown

systems.

This finding was associated with the post-fire safe shutdown category. Specifically, the

performance deficiency resulted in loss of power to equipment assumed affected in the safe

shutdown analysis and could initiate secondary fires in plant locations outside of the initial fire

area. The inspectors assigned this finding a high degradation rating since the affected circuit

breakers would not provide any fire protection benefit and would receive no fire protection

credit.

The inspectors assigned a duration factor of 1.00 since the performance deficiency existed for

greater than 30 days. The inspectors performed a Phase 1 quantitative screening using generic

fire ignition frequencies for the 13 fire areas of concern. The results of this Phase 1 screening

concluded that a Phase 2 evaluation was needed.

The inspectors followed the guidance in Manual Chapter 0609, Appendix F, Fire Protection

Significance Determination Process, to perform the Phase 2 evaluation. In accordance with

Appendix F, the inspectors used several spreadsheets from NUREG-1805, Fire Dynamics

Tools (FDTs) Quantitative Fire Hazard Analysis Methods for the U.S. Nuclear Regulatory

Commission Fire Protection Inspection Program. The inspectors used the following

spreadsheets in the Phase 2 evaluation:

02.1_Temperature_NV

02.2_Temperature_FV

05.1_Heat_Flux_Calculations_Wind_Free

9_Plume_Temperature_Calculations

10_Detector_Activation_Times

The inspectors used these spreadsheets to determine the temperature of the plume, the

temperature of the hot gas layer, and the activation time of the detection systems.

A2-2

Attachment 2

Assumptions

The inspectors used the following assumptions during the Phase 2 evaluation:

1. The inspectors assumed that the smoke detectors were located at the maximum possible

distance from the ignition source given the spacing of detectors in each fire area.

2. The inspectors assumed that the detection systems worked properly to detect the fire.

3. The inspectors assumed that the fixed suppression systems would fail to suppress the fire.

The inspectors assumed the only method of suppressing the fire was manual fire fighting by

the fire brigade.

4. The inspectors assumed that operators would take the prescribed mitigating actions during

any fire scenario that progressed to the point where the power-operated relief valve

spuriously opened and its block valve failed to close. These mitigating actions include steps

for the operators to remove the 125 Vdc control power to the train affected by the fire.

5. The licensee concluded that an inter-cable hot short in thermoset cables was needed for a

power-operated relief valve to spuriously open. Using guidance in Appendix F, Table 2.8.3,

PSP Factors Dependent on Cable Type and Failure Mode, the inspectors assumed the

conditional probability of an inter-cable hot short given a fire scenario that damaged the

thermoset cables was 0.02.

6. The licensee performed an evaluation of the equipment affected by the loss of 125 Vdc

control power. The inspectors reviewed the evaluation and concluded that the loss of

125 Vdc control power did not directly affect the equipment relied upon for post-fire safe

shutdown in each of the fire areas.

7. Without any additional knowledge of the cable routing for the set of affected equipment, the

inspectors assumed that cables for the affected equipment were routed in the same cable

trays as cables for the power-operated relief valves or the associated block valves.

8. The inspectors assumed that any equipment that experienced a loss of dc control power

would experience a short to ground that would lead to a secondary fire in another plant

location.

9. The inspectors assumed that a secondary fire in another plant location would damage the

equipment relied upon for safe shutdown in the original fire area and would lead to core

damage. As such, the inspectors provided no credit for the designated post-fire safe

shutdown equipment.

10. The inspectors assumed that the change in core damage frequency associated with the

performance deficiency resulted from the increased likelihood of secondary fires because of

the loss of circuit breaker protection.

A2-3

Attachment 2

Evaluation

During the inspection, the licensee provided information for each of the 13 fire areas, with the

exception of the reactor building, which is not readily accessible during power operations. The

information provided included the location of the power-operated relief valve cables (targets); a

description and photographs of the nearest set of ignition sources near each target; and a

discussion of the room dimensions, ventilation, and fire protection features.

The inspectors performed a field walkdown to verify the information provided by the licensee. In

particular, the inspectors verified the spatial arrangement of the fire sources and targets as well

as the distances between each source and target. The inspectors used the zone of influence

described in Appendix F, step 2.3, Fire Scenario Identification and Ignition Source Screening,

to determine the fire sources that could lead to fire scenarios that damaged the power-operated

relief valves. These scenarios involved cases where the initial fire directly damaged the cables

as well as situations where the fire propagated through a set of cable trays that contained the

power-operated relief valve cables.

The inspectors reviewed the Wolf Creek Generating Station Individual Plant Examination of

External Events, the fire hazards analysis, and drawings showing the cable routing for the

power-operated relief valves and their associated block valves inside containment. The

inspectors screened out fire scenarios involving the reactor building given the lack of ignition

sources located under the power-operated relief valve cables.

The inspectors used the Fire Dynamics Tools to calculate the temperature of the hot gas layer

in each fire area. The inspectors concluded that the hot gas layer would never reach a high

enough temperature to damage the thermoset cables. Therefore, the inspectors screened out

all fire scenarios involving a hot gas layer that would damage the power-operated relief valve.

Based on the walkdown and hot gas layer evaluations, the inspectors created an initial set of

five fire sources involving nine fire scenarios that could lead to core damage. The scenarios are

listed in the following table. The categories assigned to components and values determined

related to the Source Category, Fire Ignition Frequency, Heat Release Rate, and Severity

Factor used to characterize the fire scenarios in the significance determination process are

described in Manual Chapter 0609, Appendix F. The inspectors summarized the fire scenarios

in Table 1, Initial Fire Scenarios.

Fire Scenarios

The detailed evaluation of each ignition source is provided below. In each of these scenarios,

the inspectors used the Fire Dynamics Tools to calculate the time to damage the

power-operated relief valve and block valve cables and the time to detect the fire. As noted

above, the inspectors assumed that the fixed suppression systems failed to suppress the fire

and the only method of suppression resulted from manual fire fighting from the fire brigade.

The inspectors used Manual Chapter 0609, Appendix F, Attachment 8, Table A8.1,

Non-Suppression Probability Values for Manual Fire Fighting Based on Fire Duration Time to

Damage after Detection) and Fire Type Category to calculate the non-suppression probability

for manual fire fighting. The results are different for each scenarios based on the type of fire

and the length of time between the detection of the fire and damage to the cables.

A2-4

Attachment 2

Table 2. Initial Fire Scenarios

Scenario

Number

Ignition

Source

Source

Description

(Fire Area)

Source

Category

Initial Fire

Ignition

Frequency

Heat

Release

Rate

Severity

Factor

Fire

Targets

Nearest

Distance

1

RP-333

Relay

Panel

(A-16)

General

Control

Cabinet

6.00E-5

200 kW

0.9

4U3B

4U3A

4.8 ft

2

RP-333

Relay

Panel

(A-16)

General

Control

Cabinet

6.00E-5

650 kW

0.1

4U3B

4U3A

4.8 ft

3

SK194B

Security

Panel

(A-16)

General

Electrical

Cabinet

6.00E-5

200 kW

0.1

4U3B

4U3A

5.0 ft

4

NG01B

600 V

MCC

(A-18)

General

Electrical

Cabinet

6.00E-5

70 kW

0.9

1U3J

1U3K

3.3 ft

5

NG01B

600 V

MCC

(A-18)

General

Electrical

Cabinet

6.00E-5

200 kW

0.1

1U3J

1U3K

3.3 ft

6

Transients

C-21

Transients

(Medium)

1.70E-4

70 kW

0.9

1C8H

1C8J

1.3 ft

7

Transients

C-21

Transients

(Medium)

1.70E-4

200 kW

0.1

1C8H

1C8J

1.3 ft

8

Transients

C-22

Transients

(Medium)

1.70E-4

70 kW

0.9

4C8E

4C8F

0.0 ft

9

Transients

C-22

Transients

(Medium)

1.70E-4

200 kW

0.1

4C8E

4C8F

0.0 ft

1. Source RP-333

Panel RP-333 is a relay panel located against a wall in Fire Area A-16. The top of the cabinet is

7 10 from the floor. The inspectors treated the relay panel as a general control cabinet with a

fire ignition frequency of 6.00E-5 and heat release rates of 200 kW and 650 kW.

The power-operated relief valve cables are located in cable tray 4U3B and the power-operated

relief valve block valve cables are located in cable tray 4U3A. Cable tray 4U3B is the third tray

and cable tray 4U3A is the fourth tray from the bottom of a stack of cable trays. The lowest

cable tray is located 11 8 from the floor.

Fire Area A-16 is protected by a single zone smoke detection system with a maximum distance

of 25 feet between detectors. Areas of cable tray concentration contain preaction sprinkler

systems for fixed fire suppression.

A2-5

Attachment 2

Scenario 1 - Heat Release Rate (200 kW)

The inspectors calculated a plume temperature of 1178°F, corresponding to a damage time of 1

minute for the lowest cable tray and a damage time of 10 minutes for the target set. The

inspectors calculated a detection time less than 1 minute. The inspectors assigned a

non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes

between the time to detection and time to damage.

Scenario 2 - Heat Release Rate (650 kW)

The inspectors calculated a plume temperature exceeding 2000°F, corresponding to a damage

time of 1 minute for the lowest cable tray and a damage time of 10 minutes for the target set.

The inspectors calculated a detection time less than 1 minute. The inspectors assigned a

non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes

between the time to detection and time to damage.

2. Source SK194B

Panel SK194B is a security panel located against a wall in Fire Area A-16. The top of the

cabinet is 7 8 from the floor. The inspectors treated the security panel as a general electrical

cabinet with a fire ignition frequency of 6.00E-5 and heat release rates of 70 kW and 200 kW.

Using a zone of influence, the inspectors screened out the lower heat release rate during the

plant walkdown.

The power-operated relief valve cables are located in cable tray 4U3B and the power-operated

relief valve block valve cables are located in cable tray 4U3A. Cable tray 4U3B is the third tray

and cable tray 4U3A is the fourth tray from the bottom of a stack of cable trays. The lowest

cable tray is located 11 8 from the floor.

Fire Area A-16 is protected by a single zone smoke detection system with a maximum distance

of 25 feet between detectors. Areas of cable tray concentration contain preaction sprinkler

systems for fixed fire suppression.

Scenario 3 - Heat Release Rate (200 kW)

The inspectors calculated a plume temperature of 1103°F, corresponding to a damage time of 1

minute for the lowest cable tray and a damage time of 10 minutes for the target set. The

inspectors calculated a detection time less than 1 minute. The inspectors assigned a

non-suppression probability for manual fire fighting of 0.35 for an electrical fire with 9 minutes

between the time to detection and time to damage.

3. Source NG01B

Panel NG01B is a 600V motor control center located in the open in Fire Area A-18. The top of

the cabinet is 7 8 from the floor. The inspectors treated the motor control center as a general

electrical cabinet with a fire ignition frequency of 6.00E-5 and heat release rates of 70 kW and

200 kW.

A2-6

Attachment 2

The power-operated relief valve cables are located in cable tray 1U3J and the power-operated

relief valve block valve cables are located in cable tray 1U3K. Cable tray 1U3J is the third tray

and cable tray 1U3K is the second tray from the bottom of a stack of cable trays. The lowest

cable tray is located 9 11 from the floor.

Fire Area A-18 is protected by a cross zone smoke detection system with a maximum distance

of 5 feet between detectors. A total flooding halon system provides fixed fire suppression.

Scenario 4 - Heat Release Rate (70 kW)

The inspectors calculated a plume temperature of 421°F. Since this is less than the damage

threshold of 625 °F for thermoset cables, the inspectors screened out this scenario from further

consideration.

Scenario 5 - Heat Release Rate (200 kW)

The inspectors calculated a plume temperature of 1019°F, corresponding to a damage time of 1

minute for the lowest cable tray and a damage time of 8 minutes for the target set. The

inspectors calculated a detection time less than 1 minute. The inspectors assigned a

non-suppression probability for manual fire fighting of 0.44 for an electrical fire with 7 minutes

between the time to detection and time to damage.

4. Transient Combustibles in Fire Area C-21 (Lower Cable Spreading Room)

Fire Area C-21 has a length of 88 and a width of 66. The area is protected by a single zone

smoke detection system with a maximum distance of 15 feet between detectors. A preaction

sprinkler system provides fixed fire suppression.

The power-operated relief valve cables are located in cable tray 1C8H and the power-operated

relief valve block valve cables are located in cable tray 1C8J. Cable tray 1C8H is the fifth tray

and cable tray 1U3K is the fourth tray from the bottom of a stack of cable trays. The lowest

cable tray is located 3 4 from the floor.

The inspectors determined that the cables for both valves were located in the same cable tray

stack for approximately 107 feet and the same cable tray for approximately 8 feet. For the

Phase 2 evaluation, the inspectors conservatively assumed that the cables for both valves were

located in the lower tray through the entire area. The inspectors assumed that the cables trays

were 2 feet wide.

For the following two scenarios, the inspectors adjusted the fire ignition frequency to account for

the limited areas where a fire could damage the targets. The inspectors modified the transient

combustible fire ignition frequency by multiplying the initial fire ignition frequency by a weighting

factor. The inspectors calculated the weighting factor by dividing the surface area of the cables

trays containing cables for both valves by the area of the fire area. The inspectors calculated a

modified fire ignition frequency for transient combustibles of 6.26E-6.

Scenario 6 - Heat Release Rate (70 kW)

The inspectors calculated a plume temperature of 943°F, corresponding to a damage time of 1

minute for the lowest cable tray and a damage time of 11 minutes for the target set. The

inspectors calculated a detection time less than 1 minute. The inspectors assigned a

A2-7

Attachment 2

non-suppression probability for manual fire fighting of 0.26 for transient fires with 10 minutes

between the time to detection and time to damage.

Scenario 7 - Heat Release Rate (200 kW)

The inspectors calculated a plume temperature exceeding 2000°F, corresponding to a damage

time of 1 minute for the lowest cable tray and a damage time of 11 minutes for the target set.

The inspectors calculated a detection time less than 1 minute. The inspectors assigned a

non-suppression probability for manual fire fighting of 0.26 for transient fires with 10 minutes

between the time to detection and time to damage.

5. Transient Combustibles in Fire Area C-22 (Upper Cable Spreading Room)

Fire Area C-22 has a length of 88 and a width of 67. The power-operated relief valve cables

are located in cable trays 4C8E, 4C8F, and 4C8G and the power-operated relief valve block

valve cables are located in cable trays 4C8F and 4C8G. These cable trays transition into the

control room through the floor of the upper cable spreading room.

The inspectors determined that cables for both valves were located in the same cable tray stack

for approximately 96 feet. For the Phase 2 evaluation, the inspectors conservatively assumed

that the cables for both valves were located in the same cable tray through the entire area and

that the cable tray was located on the floor. The inspectors assumed that the cables trays were

2 feet wide.

The inspectors did not credit the detection or suppression systems for the following two

scenarios since the fire was assumed to damage the target set immediately.

For the following two scenarios, the inspectors adjusted the fire ignition frequency to account for

the limited areas where a fire could damage the targets. The inspectors modified the transient

combustible fire ignition frequency by multiplying the initial fire ignition frequency by a weighting

factor. The inspectors calculated the weighting factor by dividing the surface area of the cables

trays containing cables for both valves by the area of the fire area. The inspectors calculated a

modified fire ignition frequency for transient combustibles of 5.54E-6.

Scenario 8 - Heat Release Rate (70 kW)

The inspectors postulated that the transient fire was located on the cable tray containing the

cables for both valves, corresponding to immediate damage for the target set. The inspectors

assigned a non-suppression probability for manual fire fighting of 1.00 for transient fires with no

time between detection and damage.

Scenario 9 - Heat Release Rate (200 kW)

The inspectors postulated that the transient fire was located on the cable tray containing the

cables for both valves, corresponding to immediate damage for the target set. The inspectors

assigned a non-suppression probability for manual fire fighting of 1.00 for transient fires with no

time between detection and damage.

A2-8

Attachment 2

Results

The inspectors used the Phase 2 evaluation to perform a bounding analysis and determine an

upper limit for the change in core damage frequency. In each of the scenarios described above,

the change in core damage frequency was bounded by the conditional core damage probability

(CCDP). The inspectors calculated the conditional core damage probability using the following

equation:

Short

Hot

n

Suppressio

Non

P

x

P

x

SF

x

FIF

CCDP

=

where:

FIF denotes the fire ignition frequency

SF denotes the severity factor

n

Suppressio

Non

P

denotes the non-suppression probability

Short

Hot

P

denotes the probability of a hot short

The sum of the conditional core damage probabilities for each of the fire scenarios bounded the

total change in core damage frequency associated with this performance deficiency. The

inspectors calculated a bounding value of 6.58E-7 for the change in core damage frequency for

this performance deficiency. The results from the nine scenarios described above are

contained in the following table:

A2-9

Attachment 2

Table 3. Phase 2 Evaluation Results

Scenario

Number

Ignition

Source

Fire Ignition

Frequency

Severity

Factor

Probability of

Non-Suppression

Probability of

a Hot Short

CCDP

1

RP-333

6.00E-5

0.9

0.35

0.02

3.78E-7

2

RP-333

6.00E-5

0.1

0.35

0.02

4.20E-8

3

SK194B

6.00E-5

0.1

0.35

0.02

4.20E-8

4

NG01B

6.00E-5

0.9

N/A

N/A

N/A

5

NG01B

6.00E-5

0.1

0.44

0.02

5.28E-8

6

Transient Fire

(C-21)

6.26E-6

0.9

0.26

0.02

2.93E-8

7

Transient Fire

(C-21)

6.26E-6

0.1

0.26

0.02

3.26E-9

8

Transient Fire

(C-22)

5.54E-6

0.9

1.00

0.02

9.96E-8

9

Transient Fire

(C-22)

5.54E-6

0.1

1.00

0.02

1.11E-8

Total

6.58E-7