Information Notice 2012-21, Reactor Vessel Closure Head Studs Remain Detensioned During Plant Startup: Difference between revisions
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{{#Wiki_filter:UNITED STATES | {{#Wiki_filter:ML12264A518 UNITED STATES | ||
NUCLEAR REGULATORY COMMISSION | NUCLEAR REGULATORY COMMISSION | ||
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OFFICE OF NEW REACTORS | OFFICE OF NEW REACTORS | ||
WASHINGTON, DC 20555-0001 December 10, 2012 NRC INFORMATION NOTICE 2012-21: | WASHINGTON, DC 20555-0001 | ||
December 10, 2012 | |||
NRC INFORMATION NOTICE 2012-21: | |||
REACTOR VESSEL CLOSURE HEAD STUDS | |||
REMAIN DETENSIONED DURING PLANT | REMAIN DETENSIONED DURING PLANT | ||
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boiling-water reactor that resulted in leakage from the reactor vessel during startup operations | boiling-water reactor that resulted in leakage from the reactor vessel during startup operations | ||
and a manual scram. The NRC expects that recipients will review the information for | and a manual scram. The NRC expects that recipients will review the information for | ||
applicability to their facilities and consider actions, as appropriate, to avoid similar problems. | applicability to their facilities and consider actions, as appropriate, to avoid similar problems. | ||
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==DESCRIPTION OF CIRCUMSTANCES== | ==DESCRIPTION OF CIRCUMSTANCES== | ||
Brunswick Steam Electric Plant, Unit 2 | |||
On November 16, 2011, the Brunswick Steam Electric Plant, Unit 2 (Brunswick 2, a General | On November 16, 2011, the Brunswick Steam Electric Plant, Unit 2 (Brunswick 2, a General | ||
Electric boiling-water reactor) was in power ascension following a mid-cycle maintenance | Electric boiling-water reactor) was in power ascension following a mid-cycle maintenance | ||
outage, which required reactor vessel disassembly. Following the outage, the reactor vessel | outage, which required reactor vessel disassembly. Following the outage, the reactor vessel | ||
was reassembled and operators commenced startup operations. With the reactor in Startup | was reassembled and operators commenced startup operations. With the reactor in Startup | ||
Mode (Mode 2) and at normal operating pressure, operators noted increasing drywell floor drain | Mode (Mode 2) and at normal operating pressure, operators noted increasing drywell floor drain | ||
leakage. At 3:01 a.m. eastern standard time (EST), an Unusual Event was declared as a result | leakage. At 3:01 a.m. eastern standard time (EST), an Unusual Event was declared as a result | ||
of unidentified drywell leakage exceeding 10 gallons per minute (gpm). At 3:09 a.m. EST, a | of unidentified drywell leakage exceeding 10 gallons per minute (gpm). At 3:09 a.m. EST, a | ||
manual reactor scram was initiated from approximately 7 percent of rated thermal power due to | manual reactor scram was initiated from approximately 7 percent of rated thermal power due to | ||
the continued increase in unidentified drywell leakage. Following the scram, the reactor was | the continued increase in unidentified drywell leakage. Following the scram, the reactor was | ||
1 | depressurized and the unidentified leak rate decreased to less than 10 gpm within 1 hour. At | ||
1:45 p.m. EST on November 17, 2011, with the reactor in Cold Shutdown (Mode 4), leak investigation activities determined that the reactor vessel head studs were not fully tensioned | |||
during startup operations; therefore, an unanalyzed condition existed at Brunswick 2. | during startup operations; therefore, an unanalyzed condition existed at Brunswick 2. | ||
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Reactor vessel head stud tensioning is accomplished by attaching a tensioning device to the | Reactor vessel head stud tensioning is accomplished by attaching a tensioning device to the | ||
studs uppermost threads. Hydraulic pressure is applied to the tensioning device, which | studs uppermost threads. Hydraulic pressure is applied to the tensioning device, which | ||
stretches the stud. With the stud elongated by the tensioning device, personnel rotate the stud | stretches the stud. With the stud elongated by the tensioning device, personnel rotate the stud | ||
nut until it makes firm contact with the washer on the head flange. When the hydraulic pressure | nut until it makes firm contact with the washer on the head flange. When the hydraulic pressure | ||
is released, the nut maintains the tension and elongation in the stud, applying closure pressure | is released, the nut maintains the tension and elongation in the stud, applying closure pressure | ||
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operating the reactor vessel head stud tensioning equipment and during the validation process | operating the reactor vessel head stud tensioning equipment and during the validation process | ||
to ensure the head was properly tensioned. Following the event, the licensee assessed the | to ensure the head was properly tensioned. Following the event, the licensee assessed the | ||
stud tensioning process through equipment troubleshooting, review of the reactor vessel | stud tensioning process through equipment troubleshooting, review of the reactor vessel | ||
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reassembly procedure (Procedure 0SMP-RPV502), and interviews with refuel floor personnel. | reassembly procedure (Procedure 0SMP-RPV502), and interviews with refuel floor personnel. | ||
The equipment was found to be fully functional. However, the licensee determined that | The equipment was found to be fully functional. However, the licensee determined that | ||
personnel operating the stud tensioning equipment misinterpreted the digital display of the | personnel operating the stud tensioning equipment misinterpreted the digital display of the | ||
hydraulic pressure being applied to elongate the studs. Specifically, the licensee found that | hydraulic pressure being applied to elongate the studs. Specifically, the licensee found that | ||
personnel incorrectly believed that the actual hydraulic pressure being applied to the tensioning | personnel incorrectly believed that the actual hydraulic pressure being applied to the tensioning | ||
device was a factor of ten greater than the pressure indicated on the device. As a result, none | device was a factor of ten greater than the pressure indicated on the device. As a result, none | ||
of the 64 studs were properly tensioned during the reactor vessel assembly process. | of the 64 studs were properly tensioned during the reactor vessel assembly process. | ||
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The Stud Elongation Measurement System (SEMS III) is used at Brunswick 2 to validate proper | The Stud Elongation Measurement System (SEMS III) is used at Brunswick 2 to validate proper | ||
stud elongation. Based on interviews with personnel, the licensee determined that the refuel | stud elongation. Based on interviews with personnel, the licensee determined that the refuel | ||
floor crew incorrectly concluded that the target stud elongation value of 0.045 inches was | floor crew incorrectly concluded that the target stud elongation value of 0.045 inches was | ||
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achieved when the elongation values indicated on the SEMS III device were only between | achieved when the elongation values indicated on the SEMS III device were only between | ||
+/-0.004 inches. The licensee attributed this error to the crew incorrectly assuming that the | +/-0.004 inches. The licensee attributed this error to the crew incorrectly assuming that the | ||
elongation value of 0.045 inches was automatically deducted from the post-tensioned | elongation value of 0.045 inches was automatically deducted from the post-tensioned | ||
elongation indication on the SEMS III device. Furthermore, the elongation values of +/-0.004 inches, as indicated on the SEMS III device, correspond to the stud elongation tolerance | elongation indication on the SEMS III device. Furthermore, the elongation values of +/-0.004 inches, as indicated on the SEMS III device, correspond to the stud elongation tolerance | ||
specified in Procedure 0SMP-RPV502. Accordingly, the crew compared the low reading on the | specified in Procedure 0SMP-RPV502. Accordingly, the crew compared the low reading on the | ||
SEMS III device to the stud elongation tolerance in the procedure and erroneously determined | SEMS III device to the stud elongation tolerance in the procedure and erroneously determined | ||
that acceptable stud elongation had been achieved. The quality control inspector concurred | that acceptable stud elongation had been achieved. The quality control inspector concurred | ||
with the consensus opinion of the crew. As a result of these errors, the reactor vessel head | with the consensus opinion of the crew. As a result of these errors, the reactor vessel head | ||
studs were tensioned to only approximately 10 percent of the required amount. Therefore, Brunswick 2 reached Mode 2 with the head not properly tensioned. The increase in leakage | studs were tensioned to only approximately 10 percent of the required amount. Therefore, Brunswick 2 reached Mode 2 with the head not properly tensioned. The increase in leakage | ||
and subsequent reactor scram were a direct result of this condition. | and subsequent reactor scram were a direct result of this condition. | ||
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The licensee performed a post-event evaluation of the integrity of the reactor vessel closure | The licensee performed a post-event evaluation of the integrity of the reactor vessel closure | ||
components. The licensee concluded that no reactor coolant pressure boundary components | components. The licensee concluded that no reactor coolant pressure boundary components | ||
were damaged or overstressed as result of the event. After completing the integrity evaluation, the reactor vessel was reassembled. Prior to plant restart, a hydrostatic test was completed to | were damaged or overstressed as result of the event. After completing the integrity evaluation, the reactor vessel was reassembled. Prior to plant restart, a hydrostatic test was completed to | ||
verify that proper head stud tensioning had been achieved. The licensee attributed the root cause of this event to the failure to provide proper training and | verify that proper head stud tensioning had been achieved. The licensee attributed the root cause of this event to the failure to provide proper training and | ||
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lack of procedure guidance to correctly interpret critical data used to validate that the reactor | lack of procedure guidance to correctly interpret critical data used to validate that the reactor | ||
vessel head studs are properly tensioned. Specifically, the licensee concluded that the operator | vessel head studs are properly tensioned. Specifically, the licensee concluded that the operator | ||
errors that occurred during the reactor vessel reassembly evolution were due to an inadequate | errors that occurred during the reactor vessel reassembly evolution were due to an inadequate | ||
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understanding of the digital readings displayed on the hydraulic stud tensioning equipment and | understanding of the digital readings displayed on the hydraulic stud tensioning equipment and | ||
the SEMS III stud elongation measurement device. For both cases, the licensee determined | the SEMS III stud elongation measurement device. For both cases, the licensee determined | ||
that the crews relied on erroneous assumptions that led to incorrect conclusions. | that the crews relied on erroneous assumptions that led to incorrect conclusions. | ||
Licensee Corrective Actions | |||
The licensee revised the reactor vessel reassembly procedure (Procedure 0SMP-RPV502) to | The licensee revised the reactor vessel reassembly procedure (Procedure 0SMP-RPV502) to | ||
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The licensee also provided training to refuel floor crew personnel on the proper operation of the | The licensee also provided training to refuel floor crew personnel on the proper operation of the | ||
SEMS III and hydraulic stud tensioning equipment during reactor vessel reassembly. The | SEMS III and hydraulic stud tensioning equipment during reactor vessel reassembly. The | ||
licensee has revised its refuel floor training and qualification documents to include specific | licensee has revised its refuel floor training and qualification documents to include specific | ||
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discussion on the correct operation of the SEMS III equipment and how to properly interpret | discussion on the correct operation of the SEMS III equipment and how to properly interpret | ||
hydraulic pressure indications on the stud tensioning device. The licensee has also revised | hydraulic pressure indications on the stud tensioning device. The licensee has also revised | ||
Procedure 0SMP-RPV502 to require the necessary level of training regarding these activities, as provided in the revised training documents. In addition, the licensee has modified | Procedure 0SMP-RPV502 to require the necessary level of training regarding these activities, as provided in the revised training documents. In addition, the licensee has modified | ||
corporate-wide qualification programs for nuclear fleet refuel floor crew personnel to ensure that | corporate-wide qualification programs for nuclear fleet refuel floor crew personnel to ensure that | ||
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reactor vessel pressure test was not necessary because there are no regulatory requirements to | reactor vessel pressure test was not necessary because there are no regulatory requirements to | ||
conduct this test following mid-cycle maintenance outages. Therefore, as a corrective action, the licensee revised plant procedures to require a pressure test of the reactor vessel following | conduct this test following mid-cycle maintenance outages. Therefore, as a corrective action, the licensee revised plant procedures to require a pressure test of the reactor vessel following | ||
mid-cycle maintenance outages that require reactor vessel reassembly. | mid-cycle maintenance outages that require reactor vessel reassembly. | ||
NRC Special Inspection Team Findings | |||
An NRC special inspection team reviewed the circumstances surrounding this event. The | |||
An NRC special inspection team reviewed the circumstances surrounding this event. The | |||
inspection team reviewed the licensees actions prior to the event and identified examples of | inspection team reviewed the licensees actions prior to the event and identified examples of | ||
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improper procedure adherence that contributed to the inadequate reactor vessel head stud | improper procedure adherence that contributed to the inadequate reactor vessel head stud | ||
tensioning. Specifically, the team determined that licensee personnel failed to properly | tensioning. Specifically, the team determined that licensee personnel failed to properly | ||
pressurize the reactor vessel head stud tensioning equipment to the value specified in | pressurize the reactor vessel head stud tensioning equipment to the value specified in | ||
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Procedure 0SMP-RPV502 because the tensioning equipment operators did not know how to | Procedure 0SMP-RPV502 because the tensioning equipment operators did not know how to | ||
correctly interpret the hydraulic pressure reading on the tensioning equipment display. The | correctly interpret the hydraulic pressure reading on the tensioning equipment display. The | ||
inspection team also determined that quality control personnel failed to verify proper reactor | inspection team also determined that quality control personnel failed to verify proper reactor | ||
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vessel stud elongation in accordance with stud elongation values specified in Procedure | vessel stud elongation in accordance with stud elongation values specified in Procedure | ||
0SMP-RPV502. Further, the inspection team determined that nine of the twelve refuel floor | 0SMP-RPV502. Further, the inspection team determined that nine of the twelve refuel floor | ||
personnel performing reactor vessel reassembly did not have the necessary refuel floor support | personnel performing reactor vessel reassembly did not have the necessary refuel floor support | ||
training, as required by Procedure TRN-NGCC-1000, Conduct of Training. Finally, based on | training, as required by Procedure TRN-NGCC-1000, Conduct of Training. Finally, based on | ||
its review of Procedure 0PLP-20, Post Maintenance Testing Program, which specifies plant | its review of Procedure 0PLP-20, Post Maintenance Testing Program, which specifies plant | ||
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retaining capability of the reactor vessel following a mid-cycle maintenance outage. | retaining capability of the reactor vessel following a mid-cycle maintenance outage. | ||
The Brunswick Steam Electric Plant, Unit 2, Licensee Event Report (LER) 50-324/2-2011-002, dated January 16, 2012, contains further discussion of this event. The LER is available on the | The Brunswick Steam Electric Plant, Unit 2, Licensee Event Report (LER) 50-324/2-2011-002, dated January 16, 2012, contains further discussion of this event. The LER is available on the | ||
NRCs public Web site under Agencywide Documents Access and Management System | NRCs public Web site under Agencywide Documents Access and Management System | ||
(ADAMS) Accession No. ML12031A167. Additional information is available in NRC Special | (ADAMS) Accession No. ML12031A167. Additional information is available in NRC Special | ||
Inspection Report 05000324/2011013, dated January 25, 2012, under ADAMS Accession | Inspection Report 05000324/2011013, dated January 25, 2012, under ADAMS Accession | ||
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provide qualified personnel to operate and maintain the facility in a safe manner in all modes of | provide qualified personnel to operate and maintain the facility in a safe manner in all modes of | ||
operation. Criterion V, Instructions, Procedures, and Drawings, of Appendix B, Quality | operation. Criterion V, Instructions, Procedures, and Drawings, of Appendix B, Quality | ||
Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants, to 10 CFR Part 50 | Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants, to 10 CFR Part 50 | ||
states, in part, that instructions, procedures, or drawings shall include appropriate quantitative or | states, in part, that instructions, procedures, or drawings shall include appropriate quantitative or | ||
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guidance to correctly interpret critical indications on the stud tensioning and stud elongation | guidance to correctly interpret critical indications on the stud tensioning and stud elongation | ||
measurement equipment for verifying that proper stud tensioning had been achieved. The | measurement equipment for verifying that proper stud tensioning had been achieved. The | ||
failure to adequately tension the reactor vessel closure head studs during reactor vessel | failure to adequately tension the reactor vessel closure head studs during reactor vessel | ||
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necessary because there are no regulatory requirements to conduct this test following mid-cycle | necessary because there are no regulatory requirements to conduct this test following mid-cycle | ||
maintenance outages. However, the reactor vessel head was removed and reinstalled during | maintenance outages. However, the reactor vessel head was removed and reinstalled during | ||
this outage in the same fashion as during a refueling outage. Therefore, this event highlights | this outage in the same fashion as during a refueling outage. Therefore, this event highlights | ||
the importance of conducting mid-cycle maintenance outage activities, particularly those that | the importance of conducting mid-cycle maintenance outage activities, particularly those that | ||
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This event also highlights the importance of human performance and oversight of maintenance | This event also highlights the importance of human performance and oversight of maintenance | ||
activities. For example, operators of the stud tensioning equipment were not familiar with the | activities. For example, operators of the stud tensioning equipment were not familiar with the | ||
pressure display, yet they proceeded with tensioning based on an incorrect interpretation of | pressure display, yet they proceeded with tensioning based on an incorrect interpretation of | ||
indicated tensioner pressure. In addition, a licensee lead mechanic and a quality control | indicated tensioner pressure. In addition, a licensee lead mechanic and a quality control | ||
inspector signed a procedure checklist for stud elongation measurements using flawed data, based on incorrect explanations by other members of the maintenance crew. Other findings | inspector signed a procedure checklist for stud elongation measurements using flawed data, based on incorrect explanations by other members of the maintenance crew. Other findings | ||
related to human performance can be found in the April 20, 2012, inspection report. | related to human performance can be found in the April 20, 2012, inspection report. | ||
==CONTACT== | ==CONTACT== | ||
This IN requires no specific action or written response. Please direct any questions about this | This IN requires no specific action or written response. Please direct any questions about this | ||
matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor | matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor | ||
| Line 308: | Line 313: | ||
Regulation (NRR) or Office of New Reactors project manager. | Regulation (NRR) or Office of New Reactors project manager. | ||
/RA/ | /RA/ | ||
Timothy J. McGinty, Director | |||
/RA by JLuehman for/ | |||
Timothy J. McGinty, Director | |||
Laura A. Dudes, Director | |||
Division of Policy and Rulemaking | |||
Division of Construction Inspection | |||
Office of Nuclear Reactor Regulation | |||
and Operational Programs | |||
Office of New Reactors | Office of New Reactors | ||
Technical Contacts: | Technical Contacts: Christopher R. Sydnor, NRR | ||
Molly J. Keefe, NRR | |||
301-415-6065 | |||
301-415-5717 E-mail: | |||
E-mail | |||
Christopher.Sydnor@nrc.gov | |||
Molly.Keefe@nrc.gov | |||
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under NRC Library. | |||
ML12264A518 *via e-mail TAC No. ME8863 OFFICE | |||
EVIB:NRR | |||
AHPB:NRR | |||
Tech Editor | |||
BC:EVIB:NRR | |||
BC:AHPB:NRR | |||
NAME | |||
CSydnor* | |||
MKeefe* | |||
CHsu* | |||
SRosenberg* | |||
UShoop* | |||
DATE | |||
11/27/12 | |||
11/27/12 | |||
10/11/12 | |||
11/27/12 | |||
11/27/12 OFFICE | |||
D:DE | |||
PM:PGCB:NRR | |||
LA:PGCB:NRR | |||
BC:PGCB:NRR | |||
D:DCIP:NRO | |||
NAME | |||
PHiland (MCheok for) TAlexion | |||
CHawes | |||
DPelton (EBowman for) LDudes (JLuehman | |||
for) | |||
DATE | |||
11/27/12* | |||
11/28/12 | |||
11/29/12 | |||
11/27/12* | |||
12/03/12 OFFICE | |||
D:DPR:NRR | |||
NAME | NAME | ||
TMcGinty | |||
OFFICE | |||
12/10 /12}} | |||
{{Information notice-Nav}} | {{Information notice-Nav}} | ||
Latest revision as of 22:24, 11 January 2025
| ML12264A518 | |
| Person / Time | |
|---|---|
| Issue date: | 12/10/2012 |
| From: | Laura Dudes, Mcginty T Division of Construction Inspection and Operational Programs, Division of Policy and Rulemaking |
| To: | |
| Alexion, T | |
| References | |
| IN-12-20 | |
| Download: ML12264A518 (6) | |
ML12264A518 UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
OFFICE OF NEW REACTORS
WASHINGTON, DC 20555-0001
December 10, 2012
NRC INFORMATION NOTICE 2012-21:
REACTOR VESSEL CLOSURE HEAD STUDS
REMAIN DETENSIONED DURING PLANT
STARTUP
ADDRESSEES
All holders of an operating license or construction permit for a nuclear power reactor under
Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Domestic Licensing of
Production and Utilization Facilities, except those who have permanently ceased operations
and have certified that fuel has been permanently removed from the reactor vessel.
All holders of or applicants for an early site permit, standard design certification, standard
design approval, manufacturing license, or combined license under 10 CFR Part 52, Licenses, Certifications, and Approvals for Nuclear Power Plants.
PURPOSE
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform
addressees of an event involving detensioned reactor vessel closure head studs at a
boiling-water reactor that resulted in leakage from the reactor vessel during startup operations
and a manual scram. The NRC expects that recipients will review the information for
applicability to their facilities and consider actions, as appropriate, to avoid similar problems.
Suggestions contained in this IN are not NRC requirements; therefore, no specific action or
written response is required.
DESCRIPTION OF CIRCUMSTANCES
Brunswick Steam Electric Plant, Unit 2
On November 16, 2011, the Brunswick Steam Electric Plant, Unit 2 (Brunswick 2, a General
Electric boiling-water reactor) was in power ascension following a mid-cycle maintenance
outage, which required reactor vessel disassembly. Following the outage, the reactor vessel
was reassembled and operators commenced startup operations. With the reactor in Startup
Mode (Mode 2) and at normal operating pressure, operators noted increasing drywell floor drain
leakage. At 3:01 a.m. eastern standard time (EST), an Unusual Event was declared as a result
of unidentified drywell leakage exceeding 10 gallons per minute (gpm). At 3:09 a.m. EST, a
manual reactor scram was initiated from approximately 7 percent of rated thermal power due to
the continued increase in unidentified drywell leakage. Following the scram, the reactor was
depressurized and the unidentified leak rate decreased to less than 10 gpm within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. At
1:45 p.m. EST on November 17, 2011, with the reactor in Cold Shutdown (Mode 4), leak investigation activities determined that the reactor vessel head studs were not fully tensioned
during startup operations; therefore, an unanalyzed condition existed at Brunswick 2.
Subsequently, it was determined that none of the 64 reactor vessel head studs were adequately
tensioned.
Reactor vessel head stud tensioning is accomplished by attaching a tensioning device to the
studs uppermost threads. Hydraulic pressure is applied to the tensioning device, which
stretches the stud. With the stud elongated by the tensioning device, personnel rotate the stud
nut until it makes firm contact with the washer on the head flange. When the hydraulic pressure
is released, the nut maintains the tension and elongation in the stud, applying closure pressure
to the flanges of the reactor vessel and head.
The licensees investigation determined that this event was the result of errors made while
operating the reactor vessel head stud tensioning equipment and during the validation process
to ensure the head was properly tensioned. Following the event, the licensee assessed the
stud tensioning process through equipment troubleshooting, review of the reactor vessel
reassembly procedure (Procedure 0SMP-RPV502), and interviews with refuel floor personnel.
The equipment was found to be fully functional. However, the licensee determined that
personnel operating the stud tensioning equipment misinterpreted the digital display of the
hydraulic pressure being applied to elongate the studs. Specifically, the licensee found that
personnel incorrectly believed that the actual hydraulic pressure being applied to the tensioning
device was a factor of ten greater than the pressure indicated on the device. As a result, none
of the 64 studs were properly tensioned during the reactor vessel assembly process.
The Stud Elongation Measurement System (SEMS III) is used at Brunswick 2 to validate proper
stud elongation. Based on interviews with personnel, the licensee determined that the refuel
floor crew incorrectly concluded that the target stud elongation value of 0.045 inches was
achieved when the elongation values indicated on the SEMS III device were only between
+/-0.004 inches. The licensee attributed this error to the crew incorrectly assuming that the
elongation value of 0.045 inches was automatically deducted from the post-tensioned
elongation indication on the SEMS III device. Furthermore, the elongation values of +/-0.004 inches, as indicated on the SEMS III device, correspond to the stud elongation tolerance
specified in Procedure 0SMP-RPV502. Accordingly, the crew compared the low reading on the
SEMS III device to the stud elongation tolerance in the procedure and erroneously determined
that acceptable stud elongation had been achieved. The quality control inspector concurred
with the consensus opinion of the crew. As a result of these errors, the reactor vessel head
studs were tensioned to only approximately 10 percent of the required amount. Therefore, Brunswick 2 reached Mode 2 with the head not properly tensioned. The increase in leakage
and subsequent reactor scram were a direct result of this condition.
The licensee performed a post-event evaluation of the integrity of the reactor vessel closure
components. The licensee concluded that no reactor coolant pressure boundary components
were damaged or overstressed as result of the event. After completing the integrity evaluation, the reactor vessel was reassembled. Prior to plant restart, a hydrostatic test was completed to
verify that proper head stud tensioning had been achieved. The licensee attributed the root cause of this event to the failure to provide proper training and
lack of procedure guidance to correctly interpret critical data used to validate that the reactor
vessel head studs are properly tensioned. Specifically, the licensee concluded that the operator
errors that occurred during the reactor vessel reassembly evolution were due to an inadequate
understanding of the digital readings displayed on the hydraulic stud tensioning equipment and
the SEMS III stud elongation measurement device. For both cases, the licensee determined
that the crews relied on erroneous assumptions that led to incorrect conclusions.
Licensee Corrective Actions
The licensee revised the reactor vessel reassembly procedure (Procedure 0SMP-RPV502) to
include detailed guidance on the proper use of the SEMS III stud elongation measurement
equipment and the interpretation of hydraulic pressure indications on the stud tensioning device.
The licensee also provided training to refuel floor crew personnel on the proper operation of the
SEMS III and hydraulic stud tensioning equipment during reactor vessel reassembly. The
licensee has revised its refuel floor training and qualification documents to include specific
discussion on the correct operation of the SEMS III equipment and how to properly interpret
hydraulic pressure indications on the stud tensioning device. The licensee has also revised
Procedure 0SMP-RPV502 to require the necessary level of training regarding these activities, as provided in the revised training documents. In addition, the licensee has modified
corporate-wide qualification programs for nuclear fleet refuel floor crew personnel to ensure that
all refuel floor personnel at Brunswick maintain the necessary qualifications for performing their
assigned activities and receive the necessary level of training on the SEMS III and stud
tensioning equipment, as provided in the revised training documents.
The licensee noted that, prior to the event, a decision was made that a post maintenance
reactor vessel pressure test was not necessary because there are no regulatory requirements to
conduct this test following mid-cycle maintenance outages. Therefore, as a corrective action, the licensee revised plant procedures to require a pressure test of the reactor vessel following
mid-cycle maintenance outages that require reactor vessel reassembly.
NRC Special Inspection Team Findings
An NRC special inspection team reviewed the circumstances surrounding this event. The
inspection team reviewed the licensees actions prior to the event and identified examples of
improper procedure adherence that contributed to the inadequate reactor vessel head stud
tensioning. Specifically, the team determined that licensee personnel failed to properly
pressurize the reactor vessel head stud tensioning equipment to the value specified in
Procedure 0SMP-RPV502 because the tensioning equipment operators did not know how to
correctly interpret the hydraulic pressure reading on the tensioning equipment display. The
inspection team also determined that quality control personnel failed to verify proper reactor
vessel stud elongation in accordance with stud elongation values specified in Procedure
0SMP-RPV502. Further, the inspection team determined that nine of the twelve refuel floor
personnel performing reactor vessel reassembly did not have the necessary refuel floor support
training, as required by Procedure TRN-NGCC-1000, Conduct of Training. Finally, based on
its review of Procedure 0PLP-20, Post Maintenance Testing Program, which specifies plant
equipment shall be tested consistent with their safety functions following maintenance activities that may have impaired proper functioning of the components, the inspection team determined
that the licensee failed to specify an adequate post maintenance test to verify the pressure
retaining capability of the reactor vessel following a mid-cycle maintenance outage.
The Brunswick Steam Electric Plant, Unit 2, Licensee Event Report (LER) 50-324/2-2011-002, dated January 16, 2012, contains further discussion of this event. The LER is available on the
NRCs public Web site under Agencywide Documents Access and Management System
(ADAMS) Accession No. ML12031A167. Additional information is available in NRC Special
Inspection Report 05000324/2011013, dated January 25, 2012, under ADAMS Accession
No. ML120250556; and NRC Inspection Report 05000324/2012007, dated April 20, 2012, under
ADAMS Accession No. ML12114A036.
DISCUSSION
Section 50.120, Training and qualification of nuclear power plant personnel, of 10 CFR states, in part, that the training program must incorporate the instructional requirements necessary to
provide qualified personnel to operate and maintain the facility in a safe manner in all modes of
operation. Criterion V, Instructions, Procedures, and Drawings, of Appendix B, Quality
Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants, to 10 CFR Part 50
states, in part, that instructions, procedures, or drawings shall include appropriate quantitative or
qualitative acceptance criteria for determining that important activities have been satisfactorily
accomplished.
The root cause of this event was the failure to provide the necessary training and procedure
guidance to correctly interpret critical indications on the stud tensioning and stud elongation
measurement equipment for verifying that proper stud tensioning had been achieved. The
failure to adequately tension the reactor vessel closure head studs during reactor vessel
reassembly undermined the integrity of the reactor coolant pressure boundary, one of the
primary barriers to fission product release, during startup operations.
In addition, a decision was made that a post maintenance reactor vessel pressure test was not
necessary because there are no regulatory requirements to conduct this test following mid-cycle
maintenance outages. However, the reactor vessel head was removed and reinstalled during
this outage in the same fashion as during a refueling outage. Therefore, this event highlights
the importance of conducting mid-cycle maintenance outage activities, particularly those that
require reactor vessel disassembly and reassembly, with the same level of rigor as scheduled
refueling outage activities.
This event also highlights the importance of human performance and oversight of maintenance
activities. For example, operators of the stud tensioning equipment were not familiar with the
pressure display, yet they proceeded with tensioning based on an incorrect interpretation of
indicated tensioner pressure. In addition, a licensee lead mechanic and a quality control
inspector signed a procedure checklist for stud elongation measurements using flawed data, based on incorrect explanations by other members of the maintenance crew. Other findings
related to human performance can be found in the April 20, 2012, inspection report.
CONTACT
This IN requires no specific action or written response. Please direct any questions about this
matter to the technical contacts listed below or the appropriate Office of Nuclear Reactor
Regulation (NRR) or Office of New Reactors project manager.
/RA/
/RA by JLuehman for/
Timothy J. McGinty, Director
Laura A. Dudes, Director
Division of Policy and Rulemaking
Division of Construction Inspection
Office of Nuclear Reactor Regulation
and Operational Programs
Office of New Reactors
Technical Contacts: Christopher R. Sydnor, NRR
Molly J. Keefe, NRR
301-415-6065
301-415-5717 E-mail:
Christopher.Sydnor@nrc.gov
Molly.Keefe@nrc.gov
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under NRC Library.
ML12264A518 *via e-mail TAC No. ME8863 OFFICE
EVIB:NRR
AHPB:NRR
Tech Editor
BC:EVIB:NRR
BC:AHPB:NRR
NAME
CSydnor*
MKeefe*
CHsu*
SRosenberg*
UShoop*
DATE
11/27/12
11/27/12
10/11/12
11/27/12
11/27/12 OFFICE
D:DE
PM:PGCB:NRR
LA:PGCB:NRR
BC:PGCB:NRR
D:DCIP:NRO
NAME
PHiland (MCheok for) TAlexion
CHawes
DPelton (EBowman for) LDudes (JLuehman
for)
DATE
11/27/12*
11/28/12
11/29/12
11/27/12*
12/03/12 OFFICE
D:DPR:NRR
NAME
TMcGinty
OFFICE
12/10 /12