ML20210U294: Difference between revisions

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{{Adams
#REDIRECT [[IR 05000269/1986033]]
| number = ML20210U294
| issue date = 02/05/1987
| title = Discusses Insp Repts 50-269/86-33,50-270/86-33 & 50-287/86-33 on 861015-1110 & Forwards Notice of Violation. Test Procedure for Emergency Condenser Cooling Water Sys Inadequate to Reveal Sys Deficiencies
| author name = Grace J
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name = Tucker H
| addressee affiliation = DUKE POWER CO.
| docket = 05000269, 05000270, 05000287
| license number =
| contact person =
| document report number = NUDOCS 8702180438
| package number = ML20210U296
| document type = CORRESPONDENCE-LETTERS, NRC TO UTILITY, OUTGOING CORRESPONDENCE
| page count = 2
}}
See also: [[see also::IR 05000269/1986033]]
 
=Text=
{{#Wiki_filter:__ _.          .    . .      . _..  _.              .                        ..        - ..
      . ."                                                                            y dhu)
'
                                                    FE8 051987
            Docket Nos. 50-269, 50-270, 50-287                                                                    !
j          License Nos. DPR-38, DPR-47, DPR-55                                          .
            Duke Power Company
          96TN: Mr. H. B. Tucker, Vice President
                    Nuclear Production Department
j          422 South Church Street                                                                              '
            Charlotte, NC 28242
            Gentlemen:
                                                                                                                  ;
  '
            SUBJECT: NOTICE OF VIOLATION
]                      (INSPECTION REPORT NOS. 50-269/86-33, 50-270/86-33 AND 50-287/86-33)
                                                                                                                  ,
!          This refers to the Nuclear Regulatory Commission (NRC) inspection conducted on.                      L
!          October 15 - November 10, 1986. The inspection included a review of activities-                      '
(          authorized for your Oconee facility. At the conclusion of the inspection, the
-
            findings were discussed with those members of your staff identified in'the.
            previously forwarded inspection report. The report documenting-this inspection                        '
;          was sent to you with a letter dated December 1, 1986. NRC concerns relative to
i          the inspection findings were discussed by Dr. J. N. Grace Regional Administrator,
i          NRC, Region II, with you and members of your staff in an Enforcement Conference                      '
;          held on December 22, 1986.                                                                            -
!          The inspection findings indicate that certain. activities appeared to violate NRC
1          requirements. The violation, references to pertinent requirements, and elements
;          to be included in your response are described in the enclosed Notice of Violation.
            The violation described in the enclosed Notice of Violation involved a failure
            to satisfy a Technical Specification Limiting Condition for_0peration which .
'
                                                                                                                -;
l          required the Emergency Condenser Cooling Water _(ECCW) system to be maintained in                    ,
;          an operable condition. The violation resulted from inadequate . surveillance .
j          testing to detect degradation of the ECCW system. As discovered during a test                        1
i          conducted on October 1,1986, because of air inleakage, the ECCW system was not .
j          able to perform its required function of providing sustained siphon flow through
            the main condenser during a station blackout with the level of Lake Keowee nine                    'i
            feet below full pond. Although the system had been tested _according to the
            procedure and at the required frequency, the test procedure:was inadequate to
            reveal the system deficiencies.
:          .The ECCW system would be inoperable under the' conditions of the loss of all                        ~
            off-site and on-site power (station blackout) coincident with a low level in                          '
1
~
            Lake Keowee. Because under other conditions, suchlas a loss of just off-site
            power, the ECCW system remains operable, and the fact that sufficient water                            i
            supplies exist to provide decay heat removal even without the operation of the                        '
j          ECCW system, this violation is considered to be of low safety significance.
"
            In accordance with the " General Statement of. Policy and Procedure for NRC
            Enforcement Action," 10 CFR- Part 2 Appendix C (1986),' the violation described
[          in the enclosed Notice has been categorized as a Severity Level IV violation.~.
I
;-            8702180438 870205
              PDR    ADOCK 05000269
              G                  PDR
JH,                                                                                        l  I y T61-
                                                                                                            . .a
                    _
                                        '
    .
      1 __ .          _ ._ c  . .      . _ _ _      . - _  ..._    _-      -
                                                                                          m..,
 
    .
.-
        Duke Power Company                        2
                                                                          FE8 05 387
        Although the violation was identified by the licensee with the resident
        inspectors present, the discovery of the degradation of.the ECCW system was    ;
        considered not to have been a part of the test as originally planned and      1
        previously performed and was discovered fortuitously because the test being
        conducted lasted longer than anticipated. Previous testing had not identified
        the ECCW system degradation. Therefore, this violation is being cited.
        In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2
        Title 10, Code of Federal Regulations, a copy of this letter and its enclosure
        will be placed in the NRC Public Document Room.
        The responses directed by this letter and its enclosure are not subject to the
        clearance procedures of the Office of Management and Budget as required by the
        Paperwork Reduction Act of 1980 PL 96-511.
        Should you have any questions concerning this letter, please' contact us.
                                                  Sincerely,
                                                    Original signed by
                                                      J. P. Stohr/for -
                                                  J. Nelson Grace
                                                  Regional Administrator
        Enclosure:
        Notice of Violation                                                        '
        cc w/ encl:
  @.S.Tuckman,StationManager
        bec w/ encl:
      LNRC Resident Inspector
    p.Nicolaras,NRR
  t,df. Beach, ES:HQ
        G. Jenkins, EICS
        L. Reyes, DRP
        A. Gibson DRS
        DocumentdontrolDesk
        State of North Carolina
        IE: S                  DRS    I
                                                  EI(S                  OR    If
        Beach                    Reyes          GR enk s              MWr
                              ,
                                                                            J st
        2/3 /87                2/.f /87          2/,f/7                2/ 5 /87
    6 20
      .
}}

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