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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION  
{{#Wiki_filter:UNITED STATES
REGION III 2443 WARRENVILLE ROAD, SUITE 210 LISLE, IL 60532-4352  
                            NUCLEAR REGULATORY COMMISSION
  February 10, 2009  
                                            REGION III
                                2443 WARRENVILLE ROAD, SUITE 210
  Mr. Charles G. Pardee  
                                        LISLE, IL 60532-4352
Senior Vice President, Exelon Generation Company, LLC  
                                        February 10, 2009
President and Chief Nuclear Officer (CNO), Exelon Nuclear  
Mr. Charles G. Pardee
Senior Vice President, Exelon Generation Company, LLC
President and Chief Nuclear Officer (CNO), Exelon Nuclear
4300 Winfield Road
Warrenville IL 60555
SUBJECT:        BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION
                REPORT 05000454/2008-005 05000455/2008-005
Dear Mr. Pardee:
On December 31, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an
integrated inspection at your Byron Station, Units 1 and 2. The enclosed inspection report
documents the inspection findings which were discussed on January 15, 2009, with
Mr. D. Hoots and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, two NRC-identified findings of very low safety
significance were identified. The findings involved violations of NRC requirements. However,
because of their very low safety significance, and because the issues were entered into your
corrective action program, the NRC is treating the issues as Non-Cited Violations in accordance
with Section VI.A.1 of the NRC Enforcement Policy. Furthermore, four licensee identified
violations are listed in Section 4OA7 of this report.
If you contest the subject or severity of a Non-Cited Violation, you should provide a
response within 30 days of the date of this inspection report, with the basis for your denial,
to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,
DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory
Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001; and the Resident Inspector Office at the Byron Station.


4300 Winfield Road
C. Pardee                                    -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,
its enclosure and your response (if any) will be available electronically for public inspection
in the NRC Public Document Room or from the Publicly Available Records (PARS)
component of NRC's document system (ADAMS), accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                              Sincerely,
                                              /RA/
                                              Richard A. Skokowski, Chief
                                              Branch 3
                                              Division of Reactor Projects
Docket Nos. 50-454; 50-455
License Nos. NPF-37; NPF-66
Enclosure:    Inspection Report No. 05000454/2008-005 and 05000455/2008-005
                w/Attachment: Supplemental Information
cc w/encl:    Site Vice President - Byron Station
              Plant Manager - Byron Station
              Manager Regulatory Assurance - Byron Station
              Senior Vice President - Midwest Operations
              Senior Vice President - Operations Support
              Vice President - Licensing and Regulatory Affairs
              Director - Licensing and Regulatory Affairs
              Manager Licensing - Braidwood, Byron, and LaSalle
              Associate General Counsel
              Document Control Desk - Licensing
              Assistant Attorney General
              Illinois Emergency Management Agency
              J. Klinger, State Liaison Officer,
                Illinois Emergency Management Agency
              P. Schmidt, State Liaison Officer, State of Wisconsin
              Chairman, Illinois Commerce Commission
              B. Quigley, Byron Station


Warrenville IL  60555
C. Pardee                                                                 -2-
SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT 05000454/2008-005 05000455/2008-005 Dear Mr. Pardee:
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,
On December 31, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Byron Station, Units 1 and 2.  The enclosed inspection report documents the inspection findings which were discussed on January 15, 2009, with
its enclosure and your response (if any) will be available electronically for public inspection
Mr. D. Hoots
in the NRC Public Document Room or from the Publicly Available Records (PARS)
and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. 
component of NRC's document system (ADAMS), accessible from the NRC Web site at
The inspectors reviewed selected procedures and records, observed activities, and interviewed
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
personnel.
                                                                          Sincerely,
Based on the results of this inspection, two NRC-identified findings of very low safety significance were identified.  The findings involved violations of NRC requirements.  However, because of their very low safety significance, and because the issues were entered into your
                                                                          Richard A. Skokowski, Chief
corrective action program, the NRC is treating the issues as Non-Cited Violations in accordance with Section VI.A.1 of the NRC Enforcement Policy.  Furthermore, four licensee identified violations are listed in Section 4OA7 of this report. If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial,
                                                                          Branch 3
to the U.S. Nuclear Regulatory Commission, ATTN:  Document Control Desk, Washington,
                                                                          Division of Reactor Projects
DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC
Docket Nos. 50-454; 50-455
20555-0001; and the Resident Inspector Office at the Byron Station.
License Nos. NPF-37; NPF-66
C. Pardee     -2-  
Enclosure:                Inspection Report No. 05000454/2008-005 and 05000455/2008-005
                            w/Attachment: Supplemental Information
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure and your response (if any) will be available electronically for public inspection  
cc w/encl:                Site Vice President - Byron Station
in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
                          Plant Manager - Byron Station
Sincerely,       /RA/  Richard A. Skokowski, Chief  
                          Manager Regulatory Assurance - Byron Station
Branch 3 Division of Reactor Projects Docket Nos. 50-454; 50-455  
                          Senior Vice President - Midwest Operations
License Nos. NPF-37; NPF-66  
                          Senior Vice President - Operations Support
                          Vice President - Licensing and Regulatory Affairs
                          Director - Licensing and Regulatory Affairs
                          Manager Licensing - Braidwood, Byron, and LaSalle
                          Associate General Counsel
                          Document Control Desk - Licensing
                          Assistant Attorney General
                          Illinois Emergency Management Agency
                          J. Klinger, State Liaison Officer,
                            Illinois Emergency Management Agency
                          P. Schmidt, State Liaison Officer, State of Wisconsin
                          Chairman, Illinois Commerce Commission
                          B. Quigley, Byron Station
DOCUMENT NAME: G:\1-SECY\1-WORK IN PROGRESS\BYRO 2008 005.DOC
G Publicly Available                        G Non-Publicly Available                  G Sensitive              G Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE              RIII
NAME                RSkokowski:dtp
DATE                02/10/09
                                                          OFFICIAL RECORD COPY


Enclosure: Inspection Report No. 05000454/2008-005 and 05000455/2008-005   w/Attachment: Supplemental Information cc w/encl: Site Vice President - Byron Station  Plant Manager - Byron Station
Letter to C. Pardee from R. Skokowski dated February 10, 2009
  Manager Regulatory Assurance - Byron Station
SUBJECT:       BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT
  Senior Vice President - Midwest Operations  Senior Vice President - Operations Support  Vice President - Licensing and Regulatory Affairs
              05000454/2008-005 05000455/2008-005
  Director - Licensing and Regulatory Affairs
DISTRIBUTION:
  Manager Licensing - Braidwood, Byron, and LaSalle
Tamara Bloomer
  Associate General Counsel  Document Control Desk - Licensing  Assistant Attorney General
RidsNrrDorlLpl3-2
  Illinois Emergency Management Agency
RidsNrrPMByron Resource
  J. Klinger, State Liaison Officer, 
RidsNrrDirsIrib Resource
    Illinois Emergency Management Agency
Mark Satorius
  P. Schmidt, State Liaison Officer, State of Wisconsin  Chairman, Illinois Commerce Commission  B. Quigley, Byron Station 
Kenneth OBrien
C. Pardee    -2-
Jared Heck
Allan Barker
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure and your response (if any) will be available electronically for public inspection
Carole Ariano
in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Linda Linn
Sincerely, 
Cynthia Pederson
DRPIII
Richard A. Skokowski, Chief
DRSIII
Branch 3 Division of Reactor Projects Docket Nos. 50-454; 50-455
Patricia Buckley
License Nos. NPF-37; NPF-66
Tammy Tomczak
ROPreports@nrc.gov


Enclosure: Inspection Report No. 05000454/2008-005 and 05000455/2008-005   w/Attachment: Supplemental Information cc w/encl: Site Vice President - Byron Station  Plant Manager - Byron Station  
          U. S. NUCLEAR REGULATORY COMMISSION
  Manager Regulatory Assurance - Byron Station
                            REGION III
  Senior Vice President - Midwest Operations  Senior Vice President - Operations Support  Vice President - Licensing and Regulatory Affairs
Docket Nos:          50-454; 50-455
  Director - Licensing and Regulatory Affairs
License Nos:         NPF-37; NPF-66
  Manager Licensing - Braidwood, Byron, and LaSalle
Report Nos:          05000454/2008-005 and 05000455/2008-005
  Associate General Counsel  Document Control Desk - Licensing  Assistant Attorney General
Licensee:           Exelon Generation Company, LLC
  Illinois Emergency Management Agency
Facility:           Byron Station, Units 1 and 2
  J. Klinger, State Liaison Officer,
Location:            Byron, IL
    Illinois Emergency Management Agency
Dates:              October 1, 2008, through December 31, 2008
  P. Schmidt, State Liaison Officer, State of Wisconsin  Chairman, Illinois Commerce Commission  B. Quigley, Byron Station
Inspectors:          B. Bartlett, Senior Resident Inspector
DOCUMENT NAME:  G:\1-SECY\1-WORK IN PROGRESS\BYRO 2008 005.DOC 
                    R. Ng, Resident Inspector
G Publicly Available
                    J. Cassidy, Senior Health Physicist
G Non-Publicly Available
                    A. Dunlop, Reactor Inspector
G Sensitive
                    B. Jones, Reactor Inspector
G Non-Sensitive To receive a copy of this document, indicate in the concurrence  box "C" = Copy without attach/encl "E" = Copy with attach/encl  "N" = No copy
                    D. Jones, Reactor Inspector
  OFFICE  RIII                NAME  RSkokowski:dtp
                    R. Langstaff, Reactor Inspector
      DATE  02/10/09        OFFICIAL RECORD COPY
                    D. McNeil, Reactor Inspector
 
                    R. Winter, Reactor Inspector
Letter to C. Pardee from R. Skokowski dated February 10, 2009
                    C. Thompson, Resident Inspector
                      Illinois Department of Emergency Management
SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT 
Observer:            J. Gilliam, Reactor Engineer
05000454/2008-005 05000455/2008-005 DISTRIBUTION
Approved by:         R. Skokowski, Chief
: Tamara Bloomer
                    Branch 3
                    Division of Reactor Projects
                                                                  Enclosure


RidsNrrDorlLpl3-2  
                                  TABLE OF CONTENTS
SUMMARY OF FINDINGS                1
REPORT DETAILS                      .3
Summary of Plant Status            .3
    1.            REACTOR SAFETY .....3
      1R01        Adverse Weather Protection (71111.01) .....................................................3
      1R04        Equipment Alignment (71111.04) ................................................................4
      1R05        Fire Protection (71111.05)...........................................................................4
      1R06        Flooding (71111.06) .....6
      1R07        Annual Heat Sink Performance (71111.07).................................................6
      1R11        Licensed Operator Requalification Program (71111.11) .............................7
      1R12        Maintenance Effectiveness (71111.12) .......................................................8
      1R13        Maintenance Risk Assessments and Emergent Work Control (71111.13)..9
      1R15        Operability Evaluations (71111.15) ...........................................................10
      1R18        Plant Modifications (71111.18) ..................................................................11
      1R19        Post-Maintenance Testing (71111.19) ......................................................12
      1R20        Outage Activities (71111.20) .....................................................................13
      1R22        Surveillance Testing (71111.22)................................................................15
      1EP6        Drill Evaluation (71114.06) ........................................................................18
    2.            Radiation SAFETY ........19
      2OS1        Access Control to Radiologically Significant Areas (71121.01) .................19
      2OS2        As-Low-As-Reasonably-Achievable Planning and Controls (71121.02) ...22
      4OA1        Performance Indicator Verification (71151) ...............................................23
      4OA2        Identification and Resolution of Problems (71152)....................................28
      4OA5        Other Activities 30
      4OA6        Management Meetings ..32
      4OA7        Licensee-Identified Violations....................................................................33
SUPPLEMENTAL INFORMATION            ..1
Key Points of Contact              ..1
List of Items Opened, Closed and Discussed............................................................................1
List of Documents Reviewed        ..2
                                                                                                          Enclosure
 
                                    SUMMARY OF FINDINGS
IR 05000454/2008-005, 05000454/2008-005; October 1 - December 31, 2008; Byron Station,
Units 1 & 2; Refueling and Other Outage Activities, and Access Control to Radiologically
Significant Areas.
This report covers a 3-month period of inspection by resident inspectors and announced
baseline inspections by regional inspectors. Two Green findings were identified by the
inspectors. The findings were considered to be Non-Cited Violations of NRC regulations.
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings
for which the SDP does not apply may be Green or be assigned a severity level after NRC
management review. The NRCs program for overseeing the safe operation of commercial
nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,
dated December 2006.
A.      NRC-Identified and Self-Revealed Findings
        Cornerstone: Mitigating Systems
        Green. The inspectors identified a finding of very low safety significance and associated
        Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion V, Instructions,
        Procedures, and Drawings, for the licensees failure to follow procedure BAP 1450-1,
        Access to Containment. Specifically, the inspectors determined that the licensee failed
        to remove loose debris items from Unit 2 containment prior to Mode 4 or to perform an
        engineering evaluation per procedure. The licensee entered this issue into the
        corrective action program (CAP) as Issue Report (IR) 867171, removed the loose debris,
        and completed an evaluation to verify that the containment sump was not adversely
        affected.
        The finding is more than minor because, if left uncorrected, the issue could have
        become a more significant safety concern. The inspectors evaluated the finding using
        IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial
        Screening and Characterization of Finding, dated January 10, 2008, for the Mitigating
        Systems Cornerstone. Since this finding was not a design or qualification deficiency, did
        not result in loss of system or train safety function, and was not safety significant due to
        external events, this issue is screened as very low safety significance. This finding is
        related to the Work Control component of the Human Performance cross-cutting area for
        the licensees failure to coordinate work activities and the need for work groups to
        coordinate with each other. (H.3(b)) The personnel who left the material in containment
        assumed it was acceptable as they had documented the material in a surveillance data
        sheet, and the personnel who reviewed the completed data sheet assumed the material
        had been or would be removed from containment, and none questioned the potential
        impact upon the recirculation sump screens or coordinated with each other to ensure
        resolution of the material prior to a mode change. (Section 1R20.b)
        Cornerstone: Occupational Radiation Safety
        Green. The inspectors identified a finding of very low safety significance and associated
        NCV of Technical Specification 5.4.1 for failure to implement procedures required to
        evaluate radiological hazards for airborne radioactivity. Specifically, the inspectors
                                                  1                                      Enclosure


RidsNrrPMByron Resource
  identified that the licensee failed to re-start an air sampler on the refuel floor which
  provided the only air monitoring system while workers were performing activities in the
  area. The corrective actions taken by the licensee included starting the required air
  sampler. The issue was entered in the licensees corrective action program as
  IR 828767.
  The finding is more than minor because it impacted the program and process attribute of
  the Occupational Radiation Safety Cornerstone and affected the cornerstone objective of
  ensuring adequate protection of worker health and safety from exposure to radiation, in
  that the failure to fully evaluate the radiological hazards present in work areas could
  result in unplanned exposure to workers. The finding was determined to be of very low
  safety significance because it was not an As-Low-As-Is-Reasonably-Achievable
  (ALARA) planning issue, there was no overexposure nor potential for overexposure, and
  the licensees ability to assess dose was not compromised. This finding was caused by
  inadequate self-checking and peer checking. Consequently, the cause of this deficiency
  had a cross-cutting aspect in the area of Human Performance. (H.4(a)) Specifically, the
  licensee failed to utilize human error prevention techniques commensurate with the risk
  of the task. (Section 2OS1.1)
B. Licensee-Identified Violations
  Four violations of very low safety significance that were identified by the licensee have
  been reviewed by inspectors. Corrective actions planned or taken by the licensee have
  been entered into the licensees CAP. These violations and corrective action tracking
  numbers are listed in Section 4OA7 of this report.
                                              2                                        Enclosure


RidsNrrDirsIrib Resource
                                          REPORT DETAILS
Mark Satorius
Summary of Plant Status
Kenneth OBrien
Unit 1 operated at or near full power throughout the inspection period with minor exceptions.
Jared Heck
Unit 2 operated at or near full power throughout the inspection period with one exception. Unit 2
was in a refueling outage from October 6 through October 24, 2009.
1.    REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems and Barrier Integrity
1R01 Adverse Weather Protection (71111.01)
  .1    Winter Seasonal Readiness Preparations
    a.  Inspection Scope
        The inspectors conducted a review of the licensees preparations for winter conditions to
        verify that the plants design features and implementation of procedures were sufficient
        to protect mitigating systems from the effects of adverse weather. Documentation for
        selected risk-significant systems was reviewed to ensure that these systems would
        remain functional when challenged by inclement weather. During the inspection, the
        inspectors focused on plant specific design features and the licensees procedures used
        to mitigate or respond to adverse weather conditions. Additionally, the inspectors
        reviewed the Updated Final Safety Analysis Report (UFSAR) and performance
        requirements for systems selected for inspection, and verified that operator actions were
        appropriate as specified by plant specific procedures. Cold weather protection, such as
        heat tracing and area heaters, was verified to be in operation where applicable. The
        inspectors also reviewed corrective action program (CAP) items to verify that the
        licensee was identifying adverse weather issues at an appropriate threshold and
        entering them into their CAP in accordance with station corrective action procedures.
        Specific documents reviewed during this inspection are listed in the Attachment. The
        inspectors reviews focused specifically on the following plant systems due to their risk
        significance or susceptibility to cold weather issues:
        *        Diesel Generator Ventilation; and
        *        Essential Service Water Cooling Towers.
        This inspection constituted one winter seasonal readiness preparations sample as
        defined in IP 71111.01-05.
    b.  Findings
        No findings of significance were identified.
                                                  3                                    Enclosure


Allan Barker
1R04 Equipment Alignment (71111.04)
.1  Quarterly Partial System Walkdowns
  a. Inspection Scope
      The inspectors performed partial system walkdowns of the following risk-significant
      systems:
      *        Unit 2 Train B Auxiliary Feedwater System following Refueling Outage
              Maintenance;
      *        Unit 2 Essential Service Water System Following Refueling Outage; and
      *        Unit 1 Train A Diesel Generator While Unit 1 Train B Diesel Generator was Out
              of Service.
      The inspectors selected these systems based on their risk significance relative to the
      reactor safety cornerstones at the time they were inspected. The inspectors attempted
      to identify any discrepancies that could impact the function of the system, and, therefore,
      potentially increase risk. The inspectors reviewed applicable operating procedures,
      system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
      orders, condition reports, and the impact of ongoing work activities on redundant trains
      of equipment in order to identify conditions that could have rendered the systems
      incapable of performing their intended functions. The inspectors also walked down
      accessible portions of the systems to verify system components and support equipment
      were aligned correctly and operable. The inspectors examined the material condition of
      the components and observed operating parameters of equipment to verify that there
      were no obvious deficiencies. The inspectors also verified that the licensee had properly
      identified and resolved equipment alignment problems that could cause initiating events
      or impact the capability of mitigating systems or barriers and entered them into the CAP
      with the appropriate significance characterization. Documents reviewed are listed in the
      Attachment.
      These activities constituted three partial system walkdown samples as defined in
      IP 71111.04-05.
  b. Findings
      No findings of significance were identified.
1R05 Fire Protection (71111.05)
.1  Routine Resident Inspector Tours (71111.05Q)
  a. Inspection Scope
      The inspectors conducted fire protection walkdowns that were focused on availability,
      accessibility, and the condition of firefighting equipment in the following risk-significant
      plant areas:
      *        Division 12 Switchgear Room (Zone 5.1-1);
      *        Division 21 Switchgear Room (Zone 5.6-2);
                                                  4                                      Enclosure


Carole Ariano
    *        Auxiliary Building Elevation 451 (Zone 5.6-1);
Linda Linn Cynthia Pederson
    *        Auxiliary Building Elevation 426 (Zone 5.1-1);
    *        Auxiliary Building Elevation 426 (Zone 5.2-1); and
    *        Auxiliary Building Elevation 383 (Zone 11.4-0).
    The inspectors reviewed areas to assess if the licensee had implemented a fire
    protection program that adequately controlled combustibles and ignition sources within
    the plant, effectively maintained fire detection and suppression capability, maintained
    passive fire protection features in good material condition, and had implemented
    adequate compensatory measures for out of service, degraded or inoperable fire
    protection equipment, systems, or features in accordance with the licensees fire plan.
    The inspectors selected fire areas based on their overall contribution to internal fire risk
    as documented in the plants Individual Plant Examination of External Events with later
    additional insights, their potential to impact equipment which could initiate or mitigate a
    plant transient, or their impact on the plants ability to respond to a security event. Using
    the documents listed in the Attachment, the inspectors verified that fire hoses and
    extinguishers were in their designated locations and available for immediate use; that
    fire detectors and sprinklers were unobstructed, that transient material loading was
    within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
    be in satisfactory condition. The inspectors also verified that minor issues identified
    during the inspection were entered into the licensees CAP.
    These activities constituted six quarterly fire protection inspection samples as defined in
    IP 71111.05-05.
  b. Findings
    No findings of significance were identified.
.2  Annual Fire Protection Drill Observation (71111.05A)
  a. Inspection Scope
    On September 14 and 21, 2008, the inspectors observed a fire brigade activation for a
    Security Diesel Charger Fire. Based on this observation, the inspectors evaluated the
    readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee
    staff identified deficiencies; openly discussed them in a self-critical manner at the drill
    debrief, and took appropriate corrective actions. Specific attributes evaluated were:
    (1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper
    use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;
    (4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade
    leader communications, command, and control; (6) search for victims and propagation of
    the fire into other plant areas; (7) smoke removal operations; (8) utilization of pre
    planned strategies; (9) adherence to the pre-planned drill scenario; and (10) drill
    objectives. In addition, the inspectors evaluated the fire brigades training qualification
    and the licensees self-contained breathing apparatus inspection and maintenance
    program. Documents reviewed are listed in the Attachment to this report.
    These activities constituted one annual fire protection inspection sample as defined by
    IP 71111.05-05.
                                                5                                        Enclosure
 
  b. Findings
      No findings of significance were identified.
1R06 Flooding (71111.06)
.1  Internal Flooding
  a. Inspection Scope
      The inspectors reviewed selected risk important plant design features and licensee
      procedures intended to protect the plant and its safety related equipment from internal
      flooding events. The inspectors reviewed flood analyses and design documents,
      including the UFSAR, engineering calculations, and abnormal operating procedures to
      identify licensee commitments. The specific documents reviewed are listed in the
      Attachment to this report. In addition, the inspectors reviewed licensee drawings to
      identify areas and equipment that may be affected by internal flooding caused by the
      failure or misalignment of nearby sources of water, such as the fire suppression or the
      circulating water systems. The inspectors also reviewed the licensees corrective action
      documents with respect to past flood-related items identified in the corrective action
      program to verify the adequacy of the corrective actions. The inspectors performed a
      walkdown of the following plant area(s) to assess the adequacy of watertight doors and
      verify drains and sumps were clear of debris and were operable, and that the licensee
      complied with its commitments:
      *        Turbine Building Internal Flooding.
      This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
  b. Findings
      No findings of significance were identified.
1R07 Annual Heat Sink Performance (71111.07)
.1  Heat Sink Performance
  a. Inspection Scope
      The inspectors reviewed the licensees testing of Unit 2 Train B Diesel Generator Jacket
      Water Heat Exchanger and Unit 2 Train C Reactor Containment Fan Cooler (RCFC)
      Heat Exchanger to verify that potential deficiencies did not mask the licensees ability to
      detect degraded performance, to identify any common cause issues that had the
      potential to increase risk, and to ensure that the licensee was adequately addressing
      problems that could result in initiating events that would cause an increase in risk. The
      inspectors reviewed the licensees observations as compared against acceptance
      criteria, the correlation of scheduled testing and the frequency of testing, and the impact
      of instrument inaccuracies on test results. Inspectors also verified that test acceptance
      criteria considered differences between test conditions, design conditions, and testing
      conditions. Documents reviewed are listed in the Attachment to this report.
                                                6                                      Enclosure


DRPIII
      This annual heat sink performance inspection constituted two samples as defined in
DRSIII
      IP 71111.07-05.
Patricia Buckley Tammy Tomczak ROPreports@nrc.gov
  b. Findings
Enclosure
      No findings of significance were identified.
  U. S. NUCLEAR REGULATORY COMMISSION REGION III Docket Nos: 50-454; 50-455 License Nos: NPF-37; NPF-66 Report Nos: 05000454/2008-005 and 05000455/2008-005
1R11 Licensed Operator Requalification Program (71111.11)
Licensee: Exelon Generation Company, LLC
  .1  Resident Inspector Quarterly Review (71111.11Q)
Facility: Byron Station, Units 1 and 2
  a. Inspection Scope
Location: Byron, IL
      On November 4, 2008, the inspectors observed a crew of licensed operators in the
Dates: October 1, 2008, through December 31, 2008 Inspectors: B. Bartlett, Senior Resident Inspector  R. Ng, Resident Inspector
      plants simulator during licensed operator requalification examinations to verify that
J. Cassidy, Senior Health Physicist
      operator performance was adequate, evaluators were identifying and documenting crew
A. Dunlop, Reactor Inspector
      performance problems, and training was being conducted in accordance with licensee
B. Jones, Reactor Inspector  D. Jones, Reactor Inspector R. Langstaff, Reactor Inspector
      procedures. The inspectors evaluated the following areas:
D. McNeil, Reactor Inspector
      *        licensed operator performance;
R. Winter, Reactor Inspector
      *        crews clarity and formality of communications;
C. Thompson, Resident Inspector    Illinois Department of Emergency Management
      *        ability to take timely actions in the conservative direction;
      *        prioritization, interpretation, and verification of annunciator alarms;
Observer: J. Gilliam, Reactor Engineer
      *        correct use and implementation of abnormal and emergency procedures;
      *        control board manipulations;
      *        oversight and direction from supervisors; and
      *        ability to identify and implement appropriate TS actions and Emergency Plan
              actions and notifications.
      The crews performance in these areas was compared to pre-established operator action
      expectations and successful critical task completion requirements. Documents reviewed
      are listed in the Attachment to this report.
      This inspection constituted one quarterly licensed operator requalification program
      sample as defined in IP 71111.11.
  b. Findings
      No findings of significance were identified.
  .2  Licensed Operator Requalification Program (LORT)
  a. Inspection Scope
      The inspectors performed an inspection of the licensees LORT test/examination
      program for compliance with the stations Systems Approach to Training (SAT) program
      which would satisfy the requirements of 10 CFR 55.59(c)(4). The reviewed operating
      examination material consisted of six operating tests, each containing two or three
      dynamic simulator scenarios per operating test and 36 job performance measures
      (JPMs). The written examinations reviewed consisted of six written examinations, each
      including a Part A, Plant and Control Systems, and Part B, Administrative
                                                  7                                    Enclosure


      Controls/Procedure Limits. The examinations contained approximately 35 questions.
 
      The inspectors reviewed the annual requalification operating test and biennial written
Approved by: R. Skokowski, Chief
      examination material to evaluate general quality, construction, and difficulty level. The
Branch 3 Division of Reactor Projects 
      inspectors assessed the level of examination material duplication from week-to-week
Enclosure
      during the current year operating test. The examiners assessed the amount of written
  TABLE OF CONTENTS
      examination material duplication from week-to-week for the written examination
      administered in 2006. The inspectors reviewed the methodology for developing the
SUMMARY OF FINDINGS -------------------------1
      examinations, including the LORT program 2-year sample plan, probabilistic risk
REPORT DETAILS -------------------------.3
      assessment insights, previously identified operator performance deficiencies, and plant
Summary of Plant Status -------------------------.3
      modifications. The documents reviewed during this inspection are listed in the
1. REACTOR SAFETY....----------------------.3
      Attachment.
1R01 Adverse Weather Protection (71111.01).....................................................3
  b. Findings
1R04 Equipment Alignment (71111.04)................................................................4
      No findings of significance were identified.
1R05 Fire Protection (71111.05)...........................................................................4
  .Annual Operating Test Results
  1R06 Flooding (71111.06)....----------------------.6
  a. Inspection Scope
1R07 Annual Heat Sink Performance (71111.07).................................................6
      The inspectors reviewed the overall pass/fail results of the biennial written examination,
1R11 Licensed Operator Requalification Program (71111.11).............................7
      the individual JPM operating tests, and the simulator operating tests, which were
1R12 Maintenance Effectiveness (71111.12).......................................................8
      required to be given per 10 CFR 55.59(a)(2)) administered by the licensee from
1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13)..9
      September 22, 2008, through December 15, 2008, as part of the licensees operator
1R15 Operability Evaluations (71111.15)...........................................................10
      licensing requalification cycle. These results were compared to the thresholds
1R18 Plant Modifications (71111.18)..................................................................11
      established in IMC 0609, Appendix I, Licensed Operator Requalification Significance
1R19 Post-Maintenance Testing (71111.19)......................................................12
      Determination Process (SDP)." The evaluations were also performed to determine if the
1R20 Outage Activities (71111.20).....................................................................13
      licensee effectively implemented operator requalification guidelines established in
1R22 Surveillance Testing (71111.22)................................................................15
      NUREG-1021, Operator Licensing Examination Standards for Power Reactors, and
1EP6 Drill Evaluation (71114.06)........................................................................18
      Inspection Procedure 71111.11, Licensed Operator Requalification Program. The
2. Radiation SAFETY......---------------------..19
      documents reviewed during this inspection are listed in the Attachment.
2OS1 Access Control to Radiologically Significant Areas (71121.01).................19
  b. Findings
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)...22
      No findings of significance were identified.
4OA1 Performance Indicator Verification (71151)...............................................23
1R12 Maintenance Effectiveness (71111.12)
4OA2 Identification and Resolution of Problems (71152)....................................28
  .1   Routine Quarterly Evaluations (71111.12Q)
4OA5 Other Activities -------------------------30
  a. Inspection Scope
4OA6  Management Meetings---------------------..32
      The inspectors evaluated degraded performance issues involving the following risk
4OA7 Licensee-Identified Violations....................................................................33
      significant systems:
SUPPLEMENTAL INFORMATION -------------------------..1
      *      Auxiliary Building Ventilation System;
  Key Points of Contact -------------------------..1
      *      Unit 1 Train A Diesel Generator Ventilation Failure; and
List of Items Opened, Closed and Discussed............................................................................1
      *      Unit 2 Train A Diesel Generator Failure to Start During Manual Start Surveillance.
    List of Documents Reviewed -------------------------..2
                                                8                                      Enclosure
 
Enclosure
1SUMMARY OF FINDINGS IR 05000454/2008-005, 05000454/2008-005; October 1 - December 31, 2008; Byron Station, Units 1 & 2; Refueling and Other Outage Activities, and Access Control to Radiologically Significant Areas. This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors.
  Two Green findings were identified by the inspectors.  The findings were considered to be Non-Cited Violations of NRC regulations.  The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP).  Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial
nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. A. NRC-Identified and Self-Revealed Findings
Cornerstone:  Mitigating Systems


Green.  The inspectors identified a finding of very low safety significance and associated
    The inspectors reviewed events such as where ineffective equipment maintenance had
Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion V, "Instructions,  
    resulted in valid or invalid automatic actuations of engineered safeguards systems and
Procedures, and Drawings," for the licensee's failure to follow procedure BAP 1450-1,
    independently verified the licensee's actions to address system performance or condition
"Access to Containment."  Specifically, the inspectors determined that the licensee failed to remove loose debris items from Unit 2 containment prior to Mode 4 or to perform an engineering evaluation per procedure. The licensee entered this issue into the  
    problems in terms of the following:
corrective action program (CAP) as Issue Report (IR) 867171, removed the loose debris,
    *        implementing appropriate work practices;
and completed an evaluation to verify that the containment sump was not adversely
    *        identifying and addressing common cause failures;
    *        scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
    *        characterizing system reliability issues for performance;
    *        charging unavailability for performance;
    *        trending key parameters for condition monitoring;
    *        ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
    *        verifying appropriate performance criteria for structures, systems, and
              components (SSCs)/functions classified as (a)(2) or appropriate and adequate
              goals and corrective actions for systems classified as (a)(1).
    The inspectors assessed performance issues with respect to the reliability, availability,
    and condition monitoring of the system. In addition, the inspectors verified maintenance
    effectiveness issues were entered into the CAP with the appropriate significance
    characterization. Documents reviewed are listed in the Attachment to this report.
    This inspection constituted three quarterly maintenance effectiveness samples as
    defined in IP 71111.12-05.
  b. Findings
    No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
  a. Inspection Scope
    The inspectors reviewed the licensee's evaluation and management of plant risk for the
    maintenance and emergent work activities affecting risk-significant and safety-related
    equipment listed below to verify that the appropriate risk assessments were performed
    prior to removing equipment for work:
    *        Unit 0 Component Cooling Heat Exchanger Out of Service while Unit 2 Train B
              Diesel Generator was Out Of Service (OOS) and Bus Tie Breaker 12-13 was
              open;
    *        Shutdown Safety during Core Reload with Essential Service Water System
              Return X-Tie Valve & Unit 0 Component Cooling Heat Exchanger OOS
    *        Unit 2 Train A Residual Heat Removal System Work Window while Unit 2
              Component Cooling Heat Exchanger was OOS; and
    *        Unit 2 Train A Diesel Generator Failure to Start During Manual Start Surveillance.
    These activities were selected based on their potential risk significance relative to the
    reactor safety cornerstones. As applicable for each activity, the inspectors verified that
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
    and complete. When emergent work was performed, the inspectors verified that the
                                                9                                      Enclosure


affected.
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
The finding is more than minor because, if left uncorrected, the issue could have become a more significant safety concern.  The inspectors evaluated the finding using
    of maintenance work, discussed the results of the assessment with the licensee's
IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
Screening and Characterization of Finding," dated January 10, 2008, for the Mitigating
    consistent with the risk assessment. The inspectors also reviewed TS requirements and
Systems Cornerstone.  Since this finding was not a design or qualification deficiency, did not result in loss of system or train safety function, and was not safety significant due to external events, this issue is screened as very low safety significance.  This finding is related to the Work Control component of the Human Performance cross-cutting area for
    walked down portions of redundant safety systems, when applicable, to verify risk
the licensee's failure to coordinate work activities and the need for work groups to
    analysis assumptions were valid and applicable requirements were met. Documents
coordinate with each other.  (H.3(b))
    reviewed are listed in the Attachment to this report.
  The personnel who left the material in containment assumed it was acceptable as they had documented the material in a surveillance data sheet, and the personnel who reviewed the completed data sheet assumed the material had been or would be removed from containment, and none questioned the potential
    These maintenance risk assessments and emergent work control activities constituted
impact upon the recirculation sump screens or coordinated with each other to ensure
    four samples as defined in IP 71111.13-05.
resolution of the material prior to a mode change.  (Section 1R20.b) Cornerstone:  Occupational Radiation Safety
  b. Findings
Green.  The inspectors identified a finding of very low safety significance and associated NCV of Technical Specification 5.4.1 for failure to implement procedures required to
    No findings of significance were identified.
evaluate radiological hazards for airborne radioactivity.  Specifically, the inspectors 
1R15 Operability Evaluations (71111.15)
Enclosure
  a. Inspection Scope
2identified that the licensee failed to re-start an air sampler on the refuel floor which provided the only air monitoring system while workers were performing activities in the
    The inspectors reviewed the following issues:
area.  The corrective actions taken by the licensee included starting the required air sampler.  The issue was entered in the licensee's corrective action program as
    *       Unit 2 Train B Auxiliary Feedwater Pump Jacket Water System Overflow;
IR 828767.  The finding is more than minor because it impacted the program and process attribute of the Occupational Radiation Safety Cornerstone and affected the cornerstone objective of
    *        Unit 1 Loose Part Monitoring System Noise;
ensuring adequate protection of worker health and safety from exposure to radiation, in
    *       Unit 2 Train B Containment Sump Isolation Valve Motor Degradation; and
that the failure to fully evaluate the radiological hazards present in work areas could result in unplanned exposure to workers.  The finding was determined to be of very low safety significance because it was not an As-Low-As-Is-Reasonably-Achievable
    *       Unit 1 Train B Diesel Generator Cylinder and Head Indications.
(ALARA) planning issue, there was no overexposure nor potential for overexposure, and the licensee's ability to assess dose was not compromised.  This finding was caused by
    The inspectors selected these potential operability issues based on the risk-significance
inadequate self-checking and peer checking.  Consequently, the cause of this deficiency had a cross-cutting aspect in the area of Human Performance.  (H.4(a))
    of the associated components and systems. The inspectors evaluated the technical
  Specifically, the licensee failed to utilize human error prevention techniques commensurate with the risk of the task.  (Section 2OS1.1) B. Licensee-Identified Violations
    adequacy of the evaluations to ensure that TS operability was properly justified and the
Four violations of very low safety significance that were identified by the licensee have been reviewed by inspectors.  Corrective actions planned or taken by the licensee have been entered into the licensee's CAP.  These violations and corrective action tracking
    subject component or system remained available such that no unrecognized increase in
numbers are listed in Section 4OA7 of this report. 
    risk occurred. The inspectors compared the operability and design criteria in the
Enclosure
    appropriate sections of the TS and UFSAR to the licensees evaluations, to determine
3REPORT DETAILS Summary of Plant Status
    whether the components or systems were operable. Where compensatory measures
Unit 1 operated at or near full power throughout the inspection period with minor exceptions. 
    were required to maintain operability, the inspectors determined whether the measures
Unit 2 operated at or near full power throughout the inspection period with one exception.  Unit 2 was in a refueling outage from October 6 through October 24, 2009.  1. REACTOR SAFETY Cornerstones:  Initiating Events, Mitigating Systems and Barrier Integrity 1R01 Adverse Weather Protection (71111.01) .1 Winter Seasonal Readiness Preparations
    in place would function as intended and were properly controlled. The inspectors
a. Inspection Scope
    determined, where appropriate, compliance with bounding limitations associated with the
The inspectors conducted a review of the licensee's preparations for winter conditions to verify that the plant's design features and implementation of procedures were sufficient
    evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
to protect mitigating systems from the effects of adverse weather.  Documentation for
    documents to verify that the licensee was identifying and correcting any deficiencies
selected risk-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather. During the inspection, the inspectors focused on plant specific design features and the licensee's procedures used
    associated with operability evaluations. Documents reviewed are listed in the
to mitigate or respond to adverse weather conditions.  Additionally, the inspectors
    Attachment to this report.
reviewed the Updated Final Safety Analysis Report (UFSAR) and performance
    This operability inspection constituted four samples as defined in IP 71111.15-05
requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant specific procedures.  Cold weather protection, such as heat tracing and area heaters, was verified to be in operation where applicable.  The
  b. Findings
inspectors also reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and  
    No findings of significance were identified.
entering them into their CAP in accordance with station corrective action procedures.  
                                                10                                        Enclosure
Specific documents reviewed during this inspection are listed in the Attachment. The inspectors' reviews focused specifically on the following plant systems due to their risk significance or susceptibility to cold weather issues:
* Diesel Generator Ventilation; and  
* Essential Service Water Cooling Towers. This inspection constituted one winter seasonal readiness preparations sample as defined in IP 71111.01-05. b. Findings
No findings of significance were identified.
Enclosure
41R04 Equipment Alignment (71111.04) .1 Quarterly Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant systems: * Unit 2 Train B Auxiliary Feedwater System following Refueling Outage
Maintenance;  
* Unit 2 Essential Service Water System Following Refueling Outage; and  
* Unit 1 Train A Diesel Generator While Unit 1 Train B Diesel Generator was Out
of Service. The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected.  The inspectors attempted
to identify any discrepancies that could impact the function of the system, and, therefore,
potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains
of equipment in order to identify conditions that could have rendered the systems
incapable of performing their intended functions.  The inspectors also walked down
accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.  The inspectors examined the material condition of the components and observed operating parameter
s of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly  
identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP
with the appropriate significance characterization.  Documents reviewed are listed in the
Attachment. These activities constituted three partial system walkdown samples as defined in  
IP 71111.04-05. b. Findings
No findings of significance were identified. 1R05 Fire Protection (71111.05) .1 Routine Resident Inspector Tours (71111.05Q) a. Inspection Scope
The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant
plant areas:
* Division 12 Switchgear Room (Zone 5.1-1);
* Division 21 Switchgear Room (Zone 5.6-2); 
Enclosure
5* Auxiliary Building Elevation 451 (Zone 5.6-1);
* Auxiliary Building Elevation 426 (Zone 5.1-1); 
* Auxiliary Building Elevation 426 (Zone 5.2-1); and
* Auxiliary Building Elevation 383 (Zone 11.4-0). The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained
passive fire protection features in good material condition, and had implemented
adequate compensatory measures for out of service, degraded or inoperable fire
protection equipment, systems, or features in accordance with the licensee's fire plan. 
The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a
plant transient, or their impact on the plant's ability to respond to a security event. Using
the documents listed in the Attachment, the inspectors verified that fire hoses and
extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP.  These activities constituted six quarterly fire protection inspection samples as defined in
IP 71111.05-05. b. Findings
No findings of significance were identified. .2 Annual Fire Protection Drill Observation (71111.05A) a. Inspection Scope
On September 14 and 21, 2008, the inspectors observed a fire brigade activation for a
Security Diesel Charger Fire. Based on this observation, the inspectors evaluated the readiness of the plant fire brigade to fight fires.  The inspectors verified that the licensee  
staff identified deficiencies; openly discussed them in a self-critical manner at the drill
debrief, and took appropriate corrective actions.  Specific attributes evaluated were: 
(1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper
use and layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader communications, command, and control; (6) search for victims and propagation of
the fire into other plant areas; (7) smoke removal operations; (8) utilization of pre
planned strategies; (9) adherence to the pre-planned drill scenario; and (10) drill
objectives. In addition, the inspectors evaluated the fire brigade's training qualification and the licensee's self-contained breathing apparatus inspection and maintenance program.  Documents reviewed are listed in the Attachment to this report. These activities constituted one annual fire protection inspection sample as defined by
IP 71111.05-05. 
Enclosure
6b. Findings
No findings of significance were identified.
1R06 Flooding (71111.06) .1 Internal Flooding
a. Inspection Scope
The inspectors reviewed selected risk important plant design features and licensee procedures intended to protect the plant and its safety related equipment from internal
flooding events.  The inspectors reviewed flood analyses and design documents,
including the UFSAR, engineering calculations, and abnormal operating procedures to identify licensee commitments.  The specific documents reviewed are listed in the Attachment to this report. In addition, the inspectors reviewed licensee drawings to
identify areas and equipment that may be affected by internal flooding caused by the
failure or misalignment of nearby sources of water, such as the fire suppression or the
circulating water systems.  The inspectors also reviewed the licensee's corrective action documents with respect to past flood-related items identified in the corrective action program to verify the adequacy of the corrective actions.  The inspectors performed a
walkdown of the following plant area(s) to assess the adequacy of watertight doors and
verify drains and sumps were clear of debris and were operable, and that the licensee
complied with its commitments:
* Turbine Building Internal Flooding. This inspection constituted one internal flooding sample as defined in IP 71111.06-05. b. Findings
No findings of significance were identified. 1R07 Annual Heat Sink Performance (71111.07) .1 Heat Sink Performance
a. Inspection Scope
The inspectors reviewed the licensee's testing of Unit 2 Train B Diesel Generator Jacket
Water Heat Exchanger and Unit 2 Train C Reactor Containment Fan Cooler (RCFC) Heat Exchanger to verify that potential deficiencies did not mask the licensee's ability to
detect degraded performance, to identify any common cause issues that had the


potential to increase risk, and to ensure that the licensee was adequately addressing
1R18 Plant Modifications (71111.18)
problems that could result in initiating events that would cause an increase in risk. The inspectors reviewed the licensee's observations as compared against acceptance criteria, the correlation of scheduled testing and the frequency of testing, and the impact
.1  Temporary Plant Modifications
of instrument inaccuracies on test results. Inspectors also verified that test acceptance
  a. Inspection Scope
criteria considered differences between test conditions, design conditions, and testing
      The inspectors reviewed the following temporary modification:
conditions.  Documents reviewed are listed in the Attachment to this report. 
      *      Temporary Line to Connect the Drain Lines of Unit 2 A and D Reactor Coolant
Enclosure
              Pump Standpipes.
7This annual heat sink performance inspection constituted two samples as defined in
      The inspectors compared the temporary configuration change and associated
IP 71111.07-05. b. Findings
      10 CFR 50.59 screening and evaluation information against the design basis, the
No findings of significance were identified. 1R11 Licensed Operator Requalification Program (71111.11) .1 Resident Inspector Quarterly Review (71111.11Q) a. Inspection Scope
      UFSAR, and the TS, as applicable, to verify that the modification did not affect the
On November 4, 2008, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee
      operability or availability of the affected system. The inspectors also compared the
procedures. The inspectors evaluated the following areas:
      licensees information to operating experience information to ensure that lessons learned
* licensed operator performance;  
      from other utilities had been incorporated into the licensees decision to implement the
* crew's clarity and formality of communications;
      temporary modification. The inspectors verified that as applicable that the modifications
* ability to take timely actions in the conservative direction;
      operated as expected; modification testing adequately demonstrated continued system
* prioritization, interpretation, and verification of annunciator alarms;
      operability, availability, and reliability; and that operation of the modifications did not
* correct use and implementation of abnormal and emergency procedures;
      impact the operability of any interfacing systems. Lastly, the inspectors discussed the
* control board manipulations;
      temporary modification with operations, and engineering personnel to ensure that the
* oversight and direction from supervisors; and
      individuals were aware of how extended operation with the temporary modification in
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications. The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed  
      place could impact overall plant performance. Documents reviewed are listed in the
are listed in the Attachment to this report. This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11. b. Findings
      Attachment to this report.
No findings of significance were identified. .2 Licensed Operator Requalification Program (LORT)
      This inspection constituted one temporary modification sample as defined in
      IP 71111.18-05.
  b. Findings
      No findings of significance were identified.
.2   Permanent Plant Modifications
   a. Inspection Scope
   a. Inspection Scope
The inspectors performed an inspection of the licensee's LORT test/examination program for compliance with the station's Systems Approach to Training (SAT) program which would satisfy the requirements of 10 CFR 55.59(c)(4).  The reviewed operating
      The following engineering design package was reviewed and selected aspects were
examination material consisted of six operating tests, each containing two or three
      discussed with engineering personnel:
dynamic simulator scenarios per operating test and 36 job performance measures (JPMs).  The written examinations reviewed consisted of six written examinations, each including a Part A, Plant and Control Systems, and Part B, Administrative 
      *      Unit 2 Residual Heat Removal System Vent Valve Addition.
Enclosure
      This document and related documentation were reviewed for adequacy of the
8 Controls/Procedure Limits. The examinations contained approximately 35 questions.  The inspectors reviewed the annual requalification operating test and biennial written
      associated 10 CFR 50.59 safety evaluation screening, consideration of design
examination material to evaluate general quality, construction, and difficulty level.  The inspectors assessed the level of examination material duplication from week-to-week during the current year operating test. The examiners assessed the amount of written
      parameters, implementation of the modification, post-modification testing, and relevant
examination material duplication from week-to-week for the written examination
      procedures, design, and licensing documents were properly updated. The inspectors
administered in 2006.  The inspectors reviewed the methodology for developing the  
      observed ongoing and completed work activities to verify that installation was consistent
examinations, including the LORT program 2-year sample plan, probabilistic risk assessment insights, previously identified operator performance deficiencies, and plant modifications. The documents reviewed during this inspection are listed in the  
      with the design control documents. The modification added vent locations to safety
Attachment. b. Findings
      related piping in order to allow the removal of air/voids as necessary such as following
No findings of significance were identified. .3 Annual Operating Test Results
      maintenance. Documents reviewed are listed in the Attachment to this report.
                                                  11                                      Enclosure
 
    This inspection constituted one permanent plant modification sample as defined in
    IP 71111.18-05.
  b. Findings
    No findings of significance were identified.
1R19 Post-Maintenance Testing (71111.19)
   a. Inspection Scope
   a. Inspection Scope
The inspectors reviewed the overall pass/fail results of the biennial written examination, the individual JPM operating tests, and the simulator operating tests, which were
    The inspectors reviewed the following post-maintenance (PM) activities to verify that
required to be given per 10 CFR 55.59(a)(2)) administered by the licensee from
    procedures and test activities were adequate to ensure system operability and functional
September 22, 2008, through December 15, 2008, as part of the licensee's operator licensing requalification cycle.  These results were compared to the thresholds established in IMC 0609, Appendix I, "Licensed Operator Requalification Significance
    capability:
Determination Process (SDP)."  The evaluations were also performed to determine if the
    *      Unit 2 Safety Injection System Accumulator Injection Check Valve 2SI8818C
licensee effectively implemented operator requalification guidelines established in NUREG-1021, "Operator Licensing Examinat
            Repair;
ion Standards for Power Reactors," and Inspection Procedure 71111.11, "Licensed Operator Requalification Program."  The documents reviewed during this inspection are listed in the Attachment. b. Findings
    *       Unit 2 Charging/Safety Injection System Flow Balance following Outage
No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12) .1 Routine Quarterly Evaluations (71111.12Q) a. Inspection Scope
            Maintenance;
The inspectors evaluated degraded performance issues involving the following risk
    *       Unit 1 Train B Charging Pump Return to Service Following Maintenance;
significant systems:
    *       Unit 2 Train B Auxiliary Feedwater Valve Emergency Actuation Signal
* Auxiliary Building Ventilation System;  
            Verification Test;
* Unit 1 Train A Diesel Generator Ventilation Failure; and
    *      Work Order (WO) 1171264, Operate Diesel Generator 2A in Local Following
* Unit 2 Train A Diesel Generator Failure to Start During Manual Start Surveillance.
            Switch Repair;
 
    *      WO 00999110, Unit 1 Train B RCFC Following Breaker Maintenance; and
Enclosure
    *      Relay Actuation Surveillance 2BOSR 3.2.8-632A to Test Valve 2AF004A.
9The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and
    These activities were selected based upon the structure, system, or component's ability
independently verified the licensee's actions to address system performance or condition
    to impact risk. The inspectors evaluated these activities for the following (as applicable):
problems in terms of the following:  
    the effect of testing on the plant had been adequately addressed; testing was adequate
* implementing appropriate work practices;  
    for the maintenance performed; acceptance criteria were clear and demonstrated
* identifying and addressing common cause failures;
    operational readiness; test instrumentation was appropriate; tests were performed as
* scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
    written in accordance with properly reviewed and approved procedures; equipment was
* characterizing system reliability issues for performance;  
    returned to its operational status following testing (temporary modifications or jumpers
* charging unavailability for performance;  
    required for test performance were properly removed after test completion), and test
* trending key parameters for condition monitoring;  
    documentation was properly evaluated. The inspectors evaluated the activities against
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
    TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
* verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1). The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance  
    NRC generic communications to ensure that the test results adequately ensured that the
effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report. This inspection constituted three quarterly maintenance effectiveness samples as defined in IP 71111.12-05. b. Findings
    equipment met the licensing basis and design requirements. In addition, the inspectors
No findings of significance were identified. 1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) a. Inspection Scope
    reviewed corrective action documents associated with post-maintenance tests to
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related
    determine whether the licensee was identifying problems and entering them in the CAP
equipment listed below to verify that the appropriate risk assessments were performed
    and that the problems were being corrected commensurate with their importance to
    safety. Documents reviewed are listed in the Attachment to this report.
    This inspection constituted seven post-maintenance testing samples as defined in
    IP 71111.19-05.
  b. Findings
    No findings of significance were identified.
                                              12                                      Enclosure


prior to removing equipment for work:
1R20 Outage Activities (71111.20)
* Unit 0 Component Cooling Heat Exchanger Out of Service while Unit 2 Train B Diesel Generator was Out Of Service (OOS) and Bus Tie Breaker 12-13 was
  a. Inspection Scope
open; * Shutdown Safety during Core Reload with Essential Service Water System Return X-Tie Valve & Unit 0 Component Cooling Heat Exchanger OOS
    The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the
* Unit 2 Train A Residual Heat Removal System Work Window while Unit 2 Component Cooling Heat Exchanger was OOS; and  
    Unit 2 refueling outage (RFO - B2R14), conducted October 6 through October 24, 2008,
* Unit 2 Train A Diesel Generator Failure to Start During Manual Start Surveillance.  
    that the licensee had appropriately considered risk, industry experience, and previous
These activities were selected based on their potential risk significance relative to the reactor safety cornerstones.  As applicable for each activity, the inspectors verified that
    site-specific problems in developing and implementing a plan that assured maintenance
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
    of defense-in-depth. During the RFO, the inspectors observed portions of the shutdown
and complete. When emergent work was performed, the inspectors verified that the 
    and cooldown processes and monitored licensee controls over the outage activities
Enclosure
    listed below. Documents reviewed during the inspection are listed in the Attachment to
10plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's
    this report.
probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Documents
    *      Licensee configuration management, including maintenance of defense-in-depth
reviewed are listed in the Attachment to this report. These maintenance risk assessments and emergent work control activities constituted four samples as defined in IP 71111.13-05. b. Findings
            commensurate with the OSP for key safety functions and compliance with the
No findings of significance were identified. 1R15 Operability Evaluations (71111.15) a. Inspection Scope
            applicable TS when taking equipment out-of-service.
The inspectors reviewed the following issues:
    *      Implementation of clearance activities and confirmation that tags were properly
* Unit 2 Train B Auxiliary Feedwater
            hung and equipment appropriately configured to safely support the work or
Pump Jacket Water System Overflow;
            testing.
* Unit 1 Loose Part Monitoring System Noise;
    *      Installation and configuration of reactor coolant pressure, level, and temperature
* Unit 2 Train B Containment Sump Isolation Valve Motor Degradation; and
            instruments to provide accurate indication, accounting for instrument error.
* Unit 1 Train B Diesel Generator Cylinder and Head Indications. The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical
    *      Controls over the status and configuration of electrical systems to ensure that
adequacy of the evaluations to ensure that TS operability was properly justified and the
            TS and OSP requirements were met, and controls over switchyard activities.
subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensee's evaluations, to determine
    *      Monitoring of decay heat removal processes, systems, and components.
    *      Controls to ensure that outage work was not impacting the ability of the operators
            to operate the spent fuel pool cooling system.
    *      Reactor water inventory controls including flow paths, configurations, and
            alternative means for inventory addition, and controls to prevent inventory loss.
    *      Controls over activities that could affect reactivity.
    *      Refueling activities, including fuel handling.
    *      Startup and ascension to full power operation, tracking of startup prerequisites,
            walkdown of the containment to verify that debris had not been left which could
            block emergency core cooling system suction strainers, and reactor physics
            testing.
    *      Licensee identification and resolution of problems related to RFO activities.
    This inspection constituted one RFO sample as defined in IP 71111.20-05.
  b. Findings
    Introduction: The inspectors identified a finding of very low safety significance and an
    associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and
    Drawings, for the licensees failure to follow Procedure BAP 1450-1, Access to
    Containment.
    Description: On October 22, 2008, the licensee was in the process of restarting Unit 2
    from the refueling outage. The inspectors performed an assessment for loose debris
    inside of containment following the licensees completion of their readiness for changing
    from Mode 5 to Mode 4. During the assessment, the inspectors identified items that
    required removal prior to the change in mode, most of which were of a minor nature.
                                              13                                      Enclosure


whether the components or systems were
Examples included pieces of duct tape, cable ties, several signs, and some trash.
operable.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures
However, items found on the polar crane and items that had been left to support control
in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.  Additionally, the inspectors also reviewed a sampling of corrective action
rod drop timing testing were required by procedure either to be removed prior to Mode 4
documents to verify that the licensee was identifying and correcting any deficiencies
or to have an engineering analysis to support their presence inside containment in
associated with operability evaluations.  Documents reviewed are listed in the  
Mode 4 and above.
Attachment to this report. This operability inspection constituted four samples as defined in IP 71111.15-05 b. Findings
In Mode 4 and above, the licensee was required by TS to have the emergency sump
No findings of significance were identified. 
operable and thus containment cleanliness was required. At the time when the
Enclosure
inspectors performed their assessment of containment cleanliness, the licensee was in
111R18 Plant Modifications (71111.18) .1 Temporary Plant Modifications
Mode 5 but was within hours of making the change to Mode 4. Therefore, at the time of
a. Inspection Scope
identification by the inspectors, the items were not a challenge to the TS requirements
The inspectors reviewed the following temporary modification:
but should have been removed in preparation for the mode change. The items left for
* Temporary Line to Connect the Drain Lines of Unit 2 A and D Reactor Coolant Pump Standpipes.  
the control rod drop testing were evaluated by engineering to be left and found to be
acceptable. However, due to an internal licensee miss-communication, the items on the
The inspectors compared the temporary configuration change and associated
polar crane were left in place without an engineering evaluation performed. This
10 CFR 50.59 screening and evaluation information against the design basis, the  
condition was not identified until after Mode 4 was achieved. In addition, the licensees
UFSAR, and the TS, as applicable, to verify that the modification did not affect the
IR, which documented the items found by the inspectors, stated that items on the polar
operability or availability of the affected system. The inspectors also compared the licensee's information to operating experience information to ensure that lessons learned from other utilities had been incorporated into the licensee's decision to implement the  
crane were removed; when in fact, they were still on the crane.
temporary modification. The inspectors verified that as applicable that the modifications
The items that had been left through the mode change into Mode 4 were subsequently
operated as expected; modification testing adequately demonstrated continued system
evaluated by the licensee as being acceptable and not a significant challenge to blocking
operability, availability, and reliability; and that operation of the modifications did not impact the operability of any interfacing systems. Lastly, the inspectors discussed the temporary modification with operations, and engineering personnel to ensure that the
the containment recirculation sump screens following a postulated accident. After the
individuals were aware of how extended operation with the temporary modification in
final use of the polar crane, these items were removed. They consisted mainly of work
place could impact overall plant performance.
orders, copies of procedures, and fibrous rope.
  Documents reviewed are listed in the Attachment to this report. This inspection constituted one temporary modification sample as defined in
Analysis: The inspectors determined that the failure to remove loose debris items from
IP 71111.18-05. b. Findings
containment prior to Mode 4 or to perform an engineering evaluation as required by
No findings of significance were identified. .2 Permanent Plant Modifications
procedure was a performance deficiency warranting a significance determination. Using
a. Inspection Scope
IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated
The following engineering design package was reviewed and selected aspects were discussed with engineering personnel:
September 20, 2007; the inspectors concluded that the finding was greater than minor
* Unit 2 Residual Heat Removal System Vent Valve Addition. This document and related documentation were reviewed for adequacy of the associated 10 CFR 50.59 safety evaluation screening, consideration of design
because, if left uncorrected, the issue could have become a more significant safety
parameters, implementation of the modification, post-modification testing, and relevant procedures, design, and licensing documents were properly updated.  The inspectors observed ongoing and completed work activities to verify that installation was consistent with the design control documents. The modification added vent locations to safety related piping in order to allow the removal of air/voids as necessary such as following
concern. The inspectors evaluated the finding using IMC 0609, Significance
maintenance.  Documents reviewed are listed in the Attachment to this report. 
Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and
Enclosure
Characterization of Finding, dated January 10, 2008, for the Mitigating Systems
12This inspection constituted one permanent plant modification sample as defined in
Cornerstone. Since this finding was not a design or qualification deficiency, did not
IP 71111.18-05. b. Findings
result in loss of system or train safety function and was not safety significant due to
No findings of significance were identified. 1R19 Post-Maintenance Testing (71111.19) a. Inspection Scope
external events, it was screened as very low safety significance (Green).
The inspectors reviewed the following post-maintenance (PM) activities to verify that procedures and test activities were adequate to ensure system operability and functional
This finding is related to the Work Control component of the Human Performance
cross-cutting area for the licensees failure to coordinate work activities and the need for
work groups to coordinate with each other. The personnel who left the material in
containment assumed it was acceptable as they had documented the material in a
surveillance data sheet and the personnel who reviewed the completed data sheet
assumed the material had been or would be removed from containment and none
questioned the potential impact upon the recirculation sump screens or coordinated with
each other to ensure resolution of the material prior to a mode change. (H.3(b))
Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, requires, in part, that activities affecting quality shall be prescribed by
procedures and accomplished in accordance to these procedure. Byron Administrative
Procedure BAP 1450-1, Revision 37, Access to Containment, was written in
                                          14                                        Enclosure


capability:  
      accordance with Appendix B. Step 3.2.1 stated in part that, Tools and Equipment taken
* Unit 2 Safety Injection System Accumulator Injection Check Valve 2SI8818C
      into containment in Modes 1, 2, 3, or 4 will be removed when personnel exit
Repair; * Unit 2 Charging/Safety Injection System Flow Balance following Outage
      containment. Engineering evaluation and approval is required to leave materials, tools,
Maintenance;  
      and equipment unattended in containment. Contrary to the above, on
* Unit 1 Train B Charging Pump Return to Service Following Maintenance;  
      October 22, 2008, the inspectors identified that licensee personnel left material inside of
* Unit 2 Train B Auxiliary Feedwater Valve Emergency Actuation Signal
      containment in Mode 5 with the knowledge that the material would remain present in
Verification Test;  
      Mode 4 and Mode 3 and an engineering evaluation had not been performed. Because
* Work Order (WO) 1171264, Operate Diesel Generator 2A in Local Following
      this violation was of very low safety significance and was captured in the licensees
Switch Repair;  
      corrective action program (IR 835427), it is being treated as a NCV consistent with
* WO 00999110, Unit 1 Train B RCFC Following Breaker Maintenance; and  
      Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000455/2008005-01)
* Relay Actuation Surveillance 2BOSR 3.2.8-632A to Test Valve 2AF004A. These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated  
      The inspectors determined that the licensees subsequent failure to promptly correct the
operational readiness; test instrumentation was appropriate; tests were performed as
      loose debris left inside of containment even though the items had been entered into the
      corrective action system was a performance deficiency. Since this violation was
      licensee-identified, the enforcement aspect and its safety significance are described in
      Section 4OA7 of this report.
1R22 Surveillance Testing (71111.22)
.1  Routine Surveillance Testing
  a. Inspection Scope
      The inspectors reviewed the test results for the following activities to determine whether
      risk-significant systems and equipment were capable of performing their intended safety
      function and to verify testing was conducted in accordance with applicable procedural
      and TS requirements:
      *       Unit 2 Train B Diesel Generator 18-month Safety Injection Signal Override Test;
      *       Unit 2 Train B Auxiliary Feedwater Valve Verification Test;
      *       Unit 2 Train A Diesel Generator Operability Surveillance; and
      *       Unit 2 Train B Auxiliary Feedwater Pump Monthly Surveillance.
      The inspectors observed in-plant activities and reviewed procedures and associated
      records to determine the following:
      *        did preconditioning occur;
      *        were the effects of the testing adequately addressed by control room personnel
              or engineers prior to the commencement of the testing;
      *       were acceptance criteria clearly stated, demonstrated operational readiness, and
              consistent with the system design basis;
      *       plant equipment calibration was correct, accurate, and properly documented;
      *        as-left setpoints were within required ranges; and the calibration frequency were
              in accordance with TSs, the USAR, procedures, and applicable commitments;
      *        measuring and test equipment calibration was current;
      *       test equipment was used within the required range and accuracy; applicable
              prerequisites described in the test procedures were satisfied;
                                                15                                      Enclosure
 
    *      test frequencies met TS requirements to demonstrate operability and reliability;
            tests were performed in accordance with the test procedures and other
            applicable procedures; jumpers and lifted leads were controlled and restored
            where used;
    *      test data and results were accurate, complete, within limits, and valid;
    *      test equipment was removed after testing;
    *      where applicable for inservice testing activities, testing was performed in
            accordance with the applicable version of Section XI, American Society of
            Mechanical Engineers code, and reference values were consistent with the
            system design basis;
    *      where applicable, test results not meeting acceptance criteria were addressed
            with an adequate operability evaluation or the system or component was
            declared inoperable;
    *      where applicable for safety-related instrument control surveillance tests,
            reference setting data were accurately incorporated in the test procedure;
    *      where applicable, actual conditions encountering high resistance electrical
            contacts were such that the intended safety function could still be accomplished;
    *      prior procedure changes had not provided an opportunity to identify problems
            encountered during the performance of the surveillance or calibration test;
    *      equipment was returned to a position or status required to support the
            performance of its safety functions; and
    *      all problems identified during the testing were appropriately documented and
            dispositioned in the CAP.
    Documents reviewed are listed in the Attachment to this report.
    This inspection constituted four routine surveillance testing samples, as defined in
    IP 71111.22, Section -05.
  b. Findings
    No findings of significance were identified.
.2  Inservice Testing (IST) Surveillance
  a. Inspection Scope
    The inspectors reviewed the test results for the following activities to determine whether
    risk-significant systems and equipment were capable of performing their intended safety
    function and to verify testing was conducted in accordance with applicable procedural
    and TS requirements:
    *      Unit 2 Charging/Safety Injection System Flow Balance; and
    *      Unit 2 Reactor Coolant System Pressure Isolation Valve and Cold Leg Injection
            Isolation Valve Leakage Surveillance.
    The inspectors observed in-plant activities and reviewed procedures and associated
    records to determine whether: any preconditioning occurred; effects of the testing were
    adequately addressed by control room personnel or engineers prior to the
    commencement of the testing; acceptance criteria were clearly stated, demonstrated
                                              16                                      Enclosure


written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion), and test  
    operational readiness, and were consistent with the system design basis; plant
documentation was properly evaluated.  The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
    equipment calibration was correct, accurate, and properly documented; as left setpoints
NRC generic communications to ensure that the test results adequately ensured that the  
    were within required ranges; and the calibration frequency were in accordance with TSs,
equipment met the licensing basis and design requirements.  In addition, the inspectors
    the UFSAR, procedures, and applicable commitments; measuring and test equipment
reviewed corrective action documents associated with post-maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to
    calibration was current; test equipment was used within the required range and
safety. Documents reviewed are listed in the Attachment to this report. This inspection constituted seven post-maintenance testing samples as defined in  
    accuracy; applicable prerequisites described in the test procedures were satisfied; test
IP 71111.19-05. b. Findings
    frequencies met TS requirements to demonstrate operability and reliability; tests were
No findings of significance were identified.
    performed in accordance with the test procedures and other applicable procedures;
Enclosure
    jumpers and lifted leads were controlled and restored where used; test data and results
131R20 Outage Activities (71111.20) a. Inspection Scope
    were accurate, complete, within limits, and valid; test equipment was removed after
The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the  
    testing; where applicable for inservice testing activities, testing was performed in
Unit 2 refueling outage (RFO - B2R14), conducted October 6 through October 24, 2008, that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance
    accordance with the applicable version of Section XI, American Society of Mechanical
of defense-in-depth.  During the RFO, the inspectors observed portions of the shutdown
    Engineers Code, and reference values were consistent with the system design basis;
and cooldown processes and monitored licensee controls over the outage activities
    where applicable, test results not meeting acceptance criteria were addressed with an
listed below.  Documents reviewed during the inspection are listed in the Attachment to
    adequate operability evaluation or the system or component was declared inoperable;
this report.
    where applicable for safety-related instrument control surveillance tests, reference
* Licensee configuration management, including maintenance of defense-in-depth commensurate with the OSP for key safety functions and compliance with the applicable TS when taking equipment out-of-service.  
    setting data were accurately incorporated in the test procedure; where applicable, actual
* Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or  
    conditions encountering high resistance electrical contacts were such that the intended
testing. * Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error.
    safety function could still be accomplished; prior procedure changes had not provided an
* Controls over the status and configuration of electrical systems to ensure that TS and OSP requirements were met, and controls over switchyard activities.
    opportunity to identify problems encountered during the performance of the surveillance
* Monitoring of decay heat removal processes, systems, and components.
    or calibration test; equipment was returned to a position or status required to support the
* Controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system.
    performance of its safety functions; and all problems identified during the testing were
* Reactor water inventory controls including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss.
    appropriately documented and dispositioned in the corrective action program.
* Controls over activities that could affect reactivity.
    Documents reviewed are listed in the Attachment.
* Refueling activities, including fuel handling.
    This inspection constituted two inservice inspection samples as defined in Inspection
* Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the containment to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics
    Procedure 71111.22.
  b. Findings
    No findings of significance were identified.
.3  Containment Isolation Valve Testing
    The inspectors reviewed the test results for the following activity to determine whether
    the risk-significant system and equipment were capable of performing their intended
    safety function and to verify testing was conducted in accordance with applicable
    procedural and TS requirements:
    *       Local Leak Rate Test for Containment Isolation Valve 1RY8028.
    The inspectors observed in-plant activities and reviewed procedures and associated
    records to determine whether: any preconditioning occurred; effects of the testing were
    adequately addressed by control room personnel or engineers prior to the
    commencement of the testing; acceptance criteria were clearly stated, demonstrated
    operational readiness, and were consistent with the system design basis; plant
    equipment calibration was correct, accurate, and properly documented; as left setpoints
    were within required ranges; and the calibration frequency were in accordance with TSs,
    the UFSAR, procedures, and applicable commitments; measuring and test equipment
    calibration was current; test equipment was used within the required range and
    accuracy; applicable prerequisites described in the test procedures were satisfied; test
                                              17                                        Enclosure


testing. * Licensee identification and resolution of problems related to RFO activities. This inspection constituted one RFO sample as defined in IP 71111.20-05. b. Findings
      frequencies met TS requirements to demonstrate operability and reliability; tests were
Introduction:  The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," for the licensee's failure to follow Procedure BAP 1450-1, "Access to
      performed in accordance with the test procedures and other applicable procedures;
Containment." 
      jumpers and lifted leads were controlled and restored where used; test data and results
Description:  On October 22, 2008, the licensee was in the process of restarting Unit 2 from the refueling outage.  The inspectors performed an assessment for loose debris
      were accurate, complete, within limits, and valid; test equipment was removed after
inside of containment following the licensee's completion of their readiness for changing from Mode 5 to Mode 4.  During the assessment, the inspectors identified items that required removal prior to the change in mode, most of which were of a minor nature. 
      testing; where applicable, test results not meeting acceptance criteria were addressed
Enclosure
      with an adequate operability evaluation or the system or component was declared
14Examples included pieces of duct tape, cable ties, several signs, and some trash.  However, items found on the polar crane and items that had been left to support control
      inoperable; where applicable, actual conditions encountering high resistance electrical
rod drop timing testing were required by procedure either to be removed prior to Mode 4 or to have an engineering analysis to support their presence inside containment in
      contacts were such that the intended safety function could still be accomplished; prior
Mode 4 and above. In Mode 4 and above, the licensee was required by TS to have the emergency sump operable and thus containment cleanliness was required.  At the time when the
      procedure changes had not provided an opportunity to identify problems encountered
inspectors performed their assessment of containment cleanliness, the licensee was in Mode 5 but was within hours of making the change to Mode 4.  Therefore, at the time of identification by the inspectors, the items were not a challenge to the TS requirements but should have been removed in preparation for the mode change.  The items left for
      during the performance of the surveillance or calibration test; equipment was returned to
the control rod drop testing were evaluated by engineering to be left and found to be
      a position or status required to support the performance of its safety functions; and all
acceptable. However, due to an internal licensee miss-communication, the items on the
      problems identified during the testing were appropriately documented and dispositioned
polar crane were left in place without an engineering evaluation performed. This condition was not identified until after Mode 4 was achieved.  In addition, the licensee's
      in the CAP. Documents reviewed were listed in the Attachment.
IR, which documented the items found by the inspectors, stated that items on the polar crane were removed; when in fact, they were still on the crane. The items that had been left through the mode change into Mode 4 were subsequently evaluated by the licensee as being acceptable and not a significant challenge to blocking the containment recirculation sump screens following a postulated accident. After the final use of the polar crane, these items were removed. They consisted mainly of work
      This inspection constituted one containment isolation valve inspection sample as defined
orders, copies of procedures, and fibrous rope.  
      in IP 71111.22-05.
Analysis: The inspectors determined that the failure to remove loose debris items from containment prior to Mode 4 or to perform an engineering evaluation as required by
    b. Findings
procedure was a performance deficiency warranting a significance determinationUsing IMC 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening," dated September 20, 2007; the inspectors concluded that the finding was greater than minor
      No findings of significance were identified.
because, if left uncorrected, the issue could have become a more significant safety
1EP6 Drill Evaluation (71114.06)
concern.  The inspectors evaluated the finding using IMC 0609, "Significance
  .1    Emergency Preparedness Drill Observation
Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Finding," dated January 10, 2008, for the Mitigating Systems Cornerstone. Since this finding was not a design or qualification deficiency, did not
  a.  Inspection Scope
result in loss of system or train safety function and was not safety significant due to external events, it was screened as very low safety significance (Green). This finding is related to the Work Control component of the Human Performance cross-cutting area for the licensee's failure to coordinate work activities and the need for work groups to coordinate with each other.  The personnel who left the material in containment assumed it was acceptable as they had documented the material in a
      The inspectors evaluated the conduct of a licensee unannounced off-hour drive-in drill
surveillance data sheet and the personnel who reviewed the completed data sheet
      on November 12, 2008, to identify any weaknesses and deficiencies in classification,
assumed the material had been or would be removed from containment and none
      notification, and protective action recommendation development activities. The
questioned the potential impact upon the recirculation sump screens or coordinated with each other to ensure resolution of the material prior to a mode change. (H.3(b))
      inspectors observed emergency response operations in the Technical Support Center
Enforcement:  10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," requires, in part, that activi
      and Operation Support Center to determine whether the event classification,
ties affecting quality shall be prescribed by procedures and accomplished in accordance to these procedure. Byron Administrative
      notifications, protective action recommendations and associated response activities
Procedure BAP 1450-1, Revision 37, "Access to Containment," was written in 
      were performed in accordance with procedures. The inspectors also attended the
  Enclosure
      licensee drill critique to compare any inspector-observed weakness with those identified
15accordance with Appendix B. Step 3.2.1 stated in part that, "Tools and Equipment taken into containment in Modes 1, 2, 3, or 4 will be removed when personnel exit
      by the licensee staff in order to evaluate the critique and to verify whether the licensee
      staff was properly identifying weaknesses and entering them into the corrective action
      program. As part of the inspection, the inspectors reviewed the drill package and other
      documents listed in the Attachment to this report.
      This emergency preparedness drill inspection constituted one sample as defined in
      IP 71114.06-05.
  b. Findings
      No findings of significance were identified.
                                                18                                        Enclosure


containmentEngineering evaluation and approval is required to leave materials, tools, and equipment unattended in containment."  Contrary to the above, on October 22, 2008, the inspectors identified that licensee personnel left material inside of
2.    RADIATION SAFETY
containment in Mode 5 with the knowledge that the material would remain present in  
      Cornerstone: Occupational Radiation Safety
Mode 4 and Mode 3 and an engineering evaluation had not been performed. Because
2OS1 Access Control to Radiologically Significant Areas (71121.01)
this violation was of very low safety significance and was captured in the licensee's
  .1  Plant Walkdowns and Radiation Work Permit Reviews
corrective action program (IR 835427), it is being treated as a NCV consistent with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000455/2008005-01) The inspectors determined that the licensee's subsequent failure to promptly correct the loose debris left inside of containment even though the items had been entered into the corrective action system was a performance deficiency. Since this violation was
  a. Inspection Scope
licensee-identified, the enforcement aspect and its safety significance are
      The inspectors reviewed licensee controls and surveys in the following radiologically
described in Section 4OA7 of this report. 1R22 Surveillance Testing (71111.22) .1 Routine Surveillance Testing
      significant work areas within radiation areas, high radiation areas, and airborne
a. Inspection Scope
      radioactivity areas in the plant to determine if radiological controls including surveys,
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural
      postings, and barricades were acceptable:
      *        Unit 2 Containment Building; and
      *        Auxiliary Building.
      This inspection supplements the sample reported in Inspection
      Report 05000454/2008002; 05000455/2008002.
      The inspectors reviewed the radiation work permits (RWPs) and work packages used to
      access these areas and other high radiation work areas. The inspectors assessed the
      work control instructions and control barriers specified by the licensee. Electronic
      dosimeter alarm set points for both integrated dose and dose rate were evaluated for
      conformity with survey indications and plant policy. The inspectors interviewed workers
      to verify that they were aware of the actions required if their electronic dosimeters
      noticeably malfunctioned or alarmed.
      This inspection supplements the sample reported in Inspection
      Report 05000454/2008002; 05000455/2008002.
      The inspectors also reviewed the licensees physical and programmatic controls for
      highly activated and/or contaminated materials (non-fuel) stored within the spent fuel
      pool or other storage pools. Documents reviewed were listed in the Attachment.
      This inspection constitutes one sample as defined in IP 71121.01-5.
  b. Findings
      Introduction: A Green NRC-identified finding of very low safety significance and
      associated NCV of TS 5.4.1 was identified for failure to implement procedures required
      to evaluate radiological hazards for airborne radioactivity.
      Description: The inspectors identified that required air samples were not performed
      while workers in the reactor cavity were performing reactor disassembly, during the
      refueling outage in October 2008. Additionally, a continuous air sampler was not
      operating on the 426 elevation of containment.
      Airborne radioactivity surveys verify that the radiological conditions are similar to the
      conditions predicted during as-low-as-is-reasonably-achievable (ALARA) Planning.
                                                19                                        Enclosure


and TS requirements:
Air samples also validate that the controls specified in the ALARA Plan adequately
* Unit 2 Train B Diesel Generator 18-month Safety Injection Signal Override Test;
protect the workers from unnecessary radiation exposure. The evaluation of the
* Unit 2 Train B Auxiliary Feedwater Valve Verification Test;
radiological conditions associated with reactor disassembly was documented in RWP
* Unit 2 Train A Diesel Generator Operability Surveillance; and  
and ALARA Plan 10008916. The ALARA Plan required continuous air sampling in the
* Unit 2 Train B Auxiliary Feedwater Pump Monthly Surveillance. The inspectors observed in-plant activities and reviewed procedures and associated records to determine the following:  
reactor cavity in accordance with licensee Procedure RP-AA-302.Continuous air
* did preconditioning occur; 
sampling involved an air sample system consists of a pump and a filter. The filter is
* were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
changed periodically and analyzed for radioactivity deposits. On October 8, 2008, the
* were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
filter was removed during the previous shift and not replaced with a new filter. The on-
* plant equipment calibration was correct, accurate, and properly documented;
coming shift assumed that a new air sample filter was replaced and that the air sampler
* as-left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the USAR, procedures, and applicable commitments;
was returned to service. The on-coming shift allowed work crews to enter the reactor
* measuring and test equipment calibration was current;
cavity to perform reactor disassembly activities without validating this assumption.
* test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
The inspectors reviewed the corrective actions and ensured that a filter was installed
and the pump was operating before leaving containment. Additionally, the licensee
 
planned to evaluate the issue and to prescribe long-term actions to prevent recurrence.
Enclosure
Analysis: The inspectors determined that this finding was a performance deficiency
16* test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored
because licensees are required to comply with TS requirements and implement various
radiological control procedures. The inspectors also determined that the deficiency was
reasonably within the licensees ability to foresee and correct. The finding is more than
minor because it is associated with the Occupational Radiation Safety cornerstone
attribute of Program and Process and adversely affects the cornerstone objective of
protecting worker health and safety from exposure to radiation. Specifically, the failure
to perform required air sampling impacted the licensees ability to prevent an unplanned
personnel exposure. The finding was assessed using the Occupational Radiation Safety
SDP. The finding was determined to be of very low safety significance (Green), because
it was not an ALARA planning issue, there was no overexposure or potential for
overexposure, and the licensees ability to assess dose was not compromised.
As described above, this finding was caused by inadequate self-checking and peer
checking. Consequently, the cause of this finding had a cross-cutting aspect in the area
of Human Performance. Specifically, the licensee failed to utilize human error
prevention techniques commensurate with the risk of the task. (H.4(a))Enforcement:
Technical Specification 5.4.1.a. requires that the licensee establish, implement, and
maintain procedures specified in Regulatory Guide 1.33, Revision 2, Appendix A, which
specifies procedure for airborne radiation monitoring and for implementing the ALARA
program. Radiation Protection Procedure RP-AA-401, Operational ALARA Planning
and Controls, Revision 9, outlines the requirements for ALARA Plans and requires that
ALARA plans be developed and implemented. The ALARA Plan that evaluated reactor
disassembly and provided the methods and controls associated with reactor
disassembly activities was documented for RWP 10008916. One of the prescribed
controls included in this ALARA Plan required continuous air sampling in the cavity.
Because this finding is of very low safety significance and has been entered into the
licensees corrective action program as IR 828767, this violation is being treated as an
NCV, consistent with Section VI.A of the NRC Enforcement Policy.
(NCV 05000454/2008005-02; 05000455/2008005-02)
                                          20                                    Enclosure


where used;  
.2  Job-In-Progress Reviews
* test data and results were accurate, complete, within limits, and valid;
  a. Inspection Scope
* test equipment was removed after testing;  
    The inspectors observed the following two jobs that were being performed in radiation
* where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the  
    areas, airborne radioactivity areas, or high radiation areas for observation of work
    activities that presented the greatest radiological risk to workers:
    *        Cleaning and Eddy Current Testing of the Seal Table; and
    *       Dye Penetrant Testing of Reactor Head Penetration 68.
    The inspectors reviewed radiological job requirements for these activities, including
    RWP requirements and work procedure requirements and attended ALARA job
    briefings.
    This inspection supplements the sample reported in Inspection
    Report 05000454/2008002; 05000455/2008002.
    Job performance was observed with respect to the radiological control requirements to
    assess whether radiological conditions in the work area were adequately communicated
    to workers through pre-job briefings and postings. The inspectors evaluated the
    adequacy of radiological controls, including required radiation, contamination, and
    airborne surveys for system breaches; radiation protection job coverage, including any
    applicable audio and visual surveillance for remote job coverage; and contamination
    controls. Documents reviewed were listed in the Attachment.
    This inspection supplements the sample reported in Inspection
    Report 05000454/2008002; 05000455/2008002.
  b. Findings
    No findings of significance were identified.
.3  High Risk Significant, High Dose Rate, High Radiation Area, and Very High Radiation
    Area Controls
  a. Inspection Scope
    The inspectors held discussions with the Radiation Protection Manager concerning high
    dose rate, high radiation area and very high radiation area controls and procedures,
    including procedural changes that had occurred since the last inspection, in order to
    assess whether any procedure modifications substantially reduced the effectiveness and
    level of worker protection.
    The inspectors discussed with radiation protection supervisors the controls that were in
    place for special areas of the plant that had the potential to become very high radiation
    areas during certain plant operations. The inspectors assessed if plant operations
    required communication beforehand with the radiation protection group, so as to allow
    corresponding timely actions to properly post and control the radiation hazards.
    Documents reviewed were listed in the Attachment.
                                              21                                    Enclosure


system design basis;
      This inspection constitutes one sample as defined in IP 71121.01-5.
* where applicable, test results not meeting acceptance criteria were addressed
  b.  Findings
with an adequate operability evaluation or the system or component was declared inoperable;
      No findings of significance were identified.
* where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
.4    Radiation Worker Performance
* where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
  a.  Inspection Scope
* prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
      The inspectors reviewed radiological problem reports for which the cause of the event
* equipment was returned to a position or status required to support the performance of its safety functions; and
      was due to radiation worker errors to determine if there was an observable pattern
* all problems identified during the testing were appropriately documented and dispositioned in the CAP.   Documents reviewed are listed in the Attachment to this report.  
      traceable to a similar cause and to determine if this perspective matched the corrective
This inspection constituted four routine surveillance testing samples, as defined in IP 71111.22, Section -05. b. Findings
      action approach taken by the licensee to resolve the reported problems. Problems or
No findings of significance were identified. .2 Inservice Testing (IST) Surveillance
      issues with planned or completed corrective actions were discussed with the Radiation
a. Inspection Scope
      Protection Manager. Documents reviewed were listed in the Attachment.
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural
      This inspection constitutes one sample as defined in IP 71121.01-5.
and TS requirements:
  b. Findings
* Unit 2 Charging/Safety Injection System Flow Balance; and
      No findings of significance were identified.
* Unit 2 Reactor Coolant System Pressure Isolation Valve and Cold Leg Injection Isolation Valve Leakage Surveillance. The inspectors observed in-plant activities and reviewed procedures and associated records to determine whether:  any preconditioning occurred; effects of the testing were
.5    Radiation Protection Technician Proficiency
adequately addressed by control room personnel or engineers prior to the
  a. Inspection Scope
commencement of the testing; acceptance criteria were clearly stated, demonstrated 
      The inspectors reviewed radiological problem reports for which the cause of the event
Enclosure
      was radiation protection technician error to determine if there was an observable pattern
17operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints
      traceable to a similar cause and to determine if this perspective matched the corrective
were within required ranges; and the calibration frequency were in accordance with TSs, the UFSAR, procedures, and applicable commitments; measuring and test equipment calibration was current; test equipment was used within the required range and
      action approach taken by the licensee to resolve the reported problems. Documents
accuracy; applicable prerequisites described in the test procedures were satisfied; test
      reviewed were listed in the Attachment.
frequencies met TS requirements to demonstrate operability and reliability; tests were
      This inspection constitutes one sample as defined in IP 71121.01-5.
performed in accordance with the test procedures and other applicable procedures;
  b. Findings
jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable for inservice testing activities, testing was performed in
      No findings of significance were identified.
accordance with the applicable version of Section XI, American Society of Mechanical
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)
Engineers Code, and reference values were consistent with the system design basis;
.1    Radiological Work Planning
where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; where applicable for safety-related instrument control surveillance tests, reference
  a. Inspection Scope
setting data were accurately incorporated in the test procedure; where applicable, actual
      The inspectors evaluated the licensees list of work activities ranked by estimated
conditions encountering high resistance electrical contacts were such that the intended
      exposure that were in progress and reviewed the following two work activities of highest
safety function could still be accomplished; prior procedure changes had not provided an
      exposure significance:
opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the  
      *  Cleaning and Eddy Current Testing of the Seal Table; and
performance of its safety functions; and all problems identified during the testing were
      *  Dye Penetrant Testing of Reactor Head Penetration 68.
appropriately documented and dispositioned in the corrective action program.
                                                22                                      Enclosure
Documents reviewed are listed in the Attachment. This inspection constituted two inservice inspection samples as defined in Inspection
Procedure 71111.22. b. Findings
No findings of significance were identified. .3 Containment Isolation Valve Testing
The inspectors reviewed the test results for the following activity to determine whether the risk-significant system and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable
procedural and TS requirements:
* Local Leak Rate Test for Containment Isolation Valve 1RY8028. The inspectors observed in-plant activities and reviewed procedures and associated records to determine whether: any preconditioning occurred; effects of the testing were
adequately addressed by control room personnel or engineers prior to the
commencement of the testing; acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; plant equipment calibration was correct, accurate, and properly documented; as left setpoints
were within required ranges; and the calibration frequency were in accordance with TSs,
the UFSAR, procedures, and applicable commitments; measuring and test equipment
calibration was current; test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied; test 
Enclosure  
18frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures;
jumpers and lifted leads were controlled and restored where used; test data and results were accurate, complete, within limits, and valid; test equipment was removed after testing; where applicable, test results not meeting acceptance criteria were addressed


with an adequate operability evaluation or the system or component was declared
      This inspection supplements the sample reported in Inspection
inoperable; where applicable, actual conditions encountering high resistance electrical
      Report 05000454/2008002; 05000455/2008002.
contacts were such that the intended safety function could still be accomplished; prior
      For these two activities, the inspectors reviewed the ALARA work activity evaluations,
procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the performance of its safety functions; and all
      exposure estimates, and exposure mitigation requirements in order to verify that the
problems identified during the testing were appropriately documented and dispositioned
      licensee had established procedures and engineering and work controls that were based
in the CAP.  Documents reviewed were listed in the Attachment. This inspection constituted one containment isolation valve inspection sample as defined in IP 71111.22-05. b. Findings
      on sound radiation protection principles in order to achieve occupational exposures that
No findings of significance were identified. 1EP6 Drill Evaluation (71114.06) .1 Emergency Preparedness Drill Observation
      were ALARA. The inspectors also determined if the licensee had reasonably grouped
a. Inspection Scope
      the radiological work into work activities, based on historical precedence, industry
The inspectors evaluated the conduct of a licensee unannounced off-hour drive-in drill on November 12, 2008, to identify any weaknesses and deficiencies in classification,  
      norms, and/or special circumstances.
notification, and protective action recommendation development activities.  The
      This inspection supplements the sample reported in Inspection
inspectors observed emergency response operations in the Technical Support Center
      Report 05000454/2008002; 05000455/2008002.
and Operation Support Center to determine whether the event classification, notifications, protective action recommendations and associated response activities were performed in accordance with procedures. The inspectors also attended the  
      Documents reviewed were listed in the Attachment.
licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify whether the licensee
  b. Findings
staff was properly identifying weaknesses and entering them into the corrective action program. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment to this report. This emergency preparedness drill inspection constituted one sample as defined in
      No findings of significance were identified.
IP 71114.06-05. b. Findings
  .2    Radiation Worker Performance
No findings of significance were identified.  
  a. Inspection Scope
 
      Radiation worker and radiation protection technician performance was observed during
  Enclosure
      work activities being performed in radiation areas, airborne radioactivity areas, and high
192. RADIATION SAFETY Cornerstone:  Occupational Radiation Safety 2OS1 Access Control to Radiologically Significant Areas (71121.01) .1 Plant Walkdowns and Radiation Work Permit Reviews
      radiation areas that presented the greatest radiological risk to workers. The inspectors
a. Inspection Scope
      evaluated whether workers demonstrated the ALARA philosophy by being familiar with
The inspectors reviewed licensee controls and surveys in the following radiologically significant work areas within radiation areas, high radiation areas, and airborne
      the scope of the work activity and tools to be used, by utilizing ALARA low dose waiting
radioactivity areas in the plant to determine if radiological controls including surveys,
      areas, and by complying with work activity controls. Also, radiation worker training and
postings, and barricades were acceptable: 
      skill levels were reviewed to determine if they were sufficient relative to the radiological
* Unit 2 Containment Building; and
      hazards and the work involved. Documents reviewed were listed in the Attachment.
* Auxiliary Building. This inspection supplements the sample reported in Inspection Report 05000454/2008002; 05000455/2008002. The inspectors reviewed the radiation work permits (RWPs) and work packages used to access these areas and other high radiation work areas. The inspectors assessed the
      This inspection supplements the sample reported in Inspection
work control instructions and control barriers specified by the licensee.  Electronic
      Report 05000454/2008002; 05000455/2008002.
dosimeter alarm set points for both integrated dose and dose rate were evaluated for
  b.  Findings
conformity with survey indications and plant policy. The inspectors interviewed workers to verify that they were aware of the actions required if their electronic dosimeters noticeably malfunctioned or alarmed. This inspection supplements the sample reported in Inspection Report 05000454/2008002; 05000455/2008002. The inspectors also reviewed the licensee's physical and programmatic controls for highly activated and/or contaminated materials (non-fuel) stored within the spent fuel pool or other storage poolsDocuments reviewed were listed in the Attachment. This inspection constitutes one sample as defined in IP 71121.01-5. b. Findings
      No findings of significance were identified.
Introduction:  A Green NRC-identified finding of very low safety significance and associated NCV of TS 5.4.1 was identified for failure to implement procedures required to evaluate radiological hazards for airborne radioactivity.
4OA1 Performance Indicator Verification (71151)
Description:  The inspectors identified that required air samples were not performed while workers in the reactor cavity were performing reactor disassembly, during the
  .1    Mitigating Systems Performance Index - Emergency AC Power System
refueling outage in October 2008.  Additionally, a continuous air sampler was not
  a.  Inspection Scope
operating on the 426' elevation of containment.  Airborne radioactivity surveys verify
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
that the radiological conditions are similar to the conditions predicted during as-low-as-is-reasonably-achievable (ALARA) Planning. 
      Index (MSPI) - Unit 1 and Unit 2 Emergency AC Power System performance indicator
Enclosure
      for Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third
20Air samples also validate that the controls specified in the ALARA Plan adequately protect the workers from unnecessary radiation exposure. The evaluation of the
      quarter 2008. To determine the accuracy of the Performance Indicators (PI) data
radiological conditions associated with reactor disassembly was documented in RWP and ALARA Plan 10008916. The ALARA Plan required continuous air sampling in the reactor cavity in accordance with licensee Procedure RP-AA-302.Continuous air
      reported during those periods, PI definitions and guidance contained in the Nuclear
sampling involved an air sample system consists of a pump and a filterThe filter is
                                                23                                        Enclosure
changed periodically and analyzed for radioactivity deposits.  On October 8, 2008, the
filter was removed during the previous shift and not replaced with a new filter.  The on-
coming shift assumed that a new air sample filter was replaced and that the air sampler was returned to service.  The on-coming shift allowed work crews to enter the reactor cavity to perform reactor disassembly activities without validating this assumption.  The inspectors reviewed the corrective actions and ensured that a filter was installed
and the pump was operating before leaving containment.  Additionally, the licensee planned to evaluate the issue and to prescribe long-term actions to prevent recurrence.
Analysis:  The inspectors determined that this finding was a performance deficiency because licensees are required to comply with TS requirements and implement various radiological control procedures.  The inspectors also determined that the deficiency was
reasonably within the licensee's ability to foresee and correct.  The finding is more than
minor because it is associated with the
Occupational Radiation Safety cornerstone attribute of Program and Process and adversely affects the cornerstone objective of protecting worker health and safety from exposure to radiation.  Specifically, the failure
to perform required air sampling impacted the licensee's ability to prevent an unplanned personnel exposure.  The finding was assessed using the Occupational Radiation Safety
SDP.  The finding was determined to be of very low safety significance (Green), because
it was not an ALARA planning issue, there was no overexposure or potential for overexposure, and the licensee's ability to assess dose was not compromised.  As described above, this finding was caused by inadequate self-checking and peer checking.  Consequently, the cause of this finding had a cross-cutting aspect in the area
of Human Performance.  Specifically, the licensee failed to utilize human error
prevention techniques commensurate with the risk of the task.  (H.4(a))Enforcement
:  Technical Specification 5.4.1.a. requires that the licensee establish, implement, and maintain procedures specified in Regulatory Guide 1.33, Revision 2, Appendix A, which
specifies procedure for airborne radiation monitoring and for implementing the ALARA
program.  Radiation Protection Procedure RP-AA-401, "Operational ALARA Planning
and Controls," Revision 9, outlines the requirements for ALARA Plans and requires that
ALARA plans be developed and implemented.  The ALARA Plan that evaluated reactor disassembly and provided the methods and controls associated with reactor disassembly activities was documented for RWP 10008916.  One of the prescribed
controls included in this ALARA Plan required continuous air sampling in the cavity.
Because this finding is of very low safety significance and has been entered into the  
licensee's corrective action program as IR 828767, this violation is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy.  (NCV 05000454/2008005-02; 05000455/2008005-02)  
 
Enclosure
21.2 Job-In-Progress Reviews
a. Inspection Scope
The inspectors observed the following two jobs that were being performed in radiation areas, airborne radioactivity areas, or high radiation areas for observation of work activities that presented the greatest radiological risk to workers:
* Cleaning and Eddy Current Testing of the Seal Table; and
* Dye Penetrant Testing of Reactor Head Penetration 68.
The inspectors reviewed radiological job requirements for these activities, including


RWP requirements and work procedure requirements and attended ALARA job
    Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
    Guideline, Revision 5, were used. The inspectors reviewed the licensees operator
    narrative logs, MSPI derivation reports, issue reports, event reports, and NRC Integrated
    Inspection Reports for the period of October 2007 through September 2008 to validate
    the accuracy of the submittals. The inspectors reviewed the MSPI component risk
    coefficient to determine if it had changed by more than 25 percent in value since the
    previous inspection, and if so, that the change was in accordance with applicable
    NEI guidance. The inspectors also reviewed the licensees issue report database to
    determine if any problems had been identified with the PI data collected or transmitted
    for this indicator and none were identified. Documents reviewed are listed in the
    Attachment to this report.
    This inspection constituted two MSPI emergency AC power system samples as defined
    in IP 71151-05.
  b. Findings
    No findings of significance were identified.
.2  Mitigating Systems Performance Index - High Pressure Injection Systems
  a. Inspection Scope
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
    Index - Unit 1 and Unit 2 High Pressure Injection Systems performance indicator for
    Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third
    quarter 2008. To determine the accuracy of the PI data reported during those periods,
    PI definitions and guidance contained in the NEI Document 99-02, Regulatory
    Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors
    reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports,
    event reports, and NRC Integrated Inspection Reports for the period of October 2007 to
    September 2008 to validate the accuracy of the submittals. The inspectors reviewed the
    MSPI component risk coefficient to determine if it had changed by more than 25 percent
    in value since the previous inspection, and if so, that the change was in accordance with
    applicable NEI guidance. The inspectors also reviewed the licensees issue report
    database to determine if any problems had been identified with the PI data collected or
    transmitted for this indicator and none were identified. Documents reviewed are listed in
    the Attachment to this report.
    This inspection constituted two MSPI high pressure injection system samples as defined
    in IP 71151-05.
  b. Findings
    No findings of significance were identified.
                                              24                                    Enclosure


briefings.  This inspection supplements the sample reported in Inspection Report 05000454/2008002; 05000455/2008002. Job performance was observed with respect to the radiological control requirements to assess whether radiological conditions in the work area were adequately communicated
.3  Mitigating Systems Performance Index - Heat Removal System
to workers through pre-job briefings and postings.  The inspectors evaluated the
  a. Inspection Scope
adequacy of radiological controls, including required radiation, contamination, and
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
airborne surveys for system breaches; radiation protection job coverage, including any applicable audio and visual surveillance for remote job coverage; and contamination controls.  Documents reviewed were listed in the Attachment. This inspection supplements the sample reported in Inspection Report 05000454/2008002; 05000455/2008002. b. Findings
    Index - Unit 1 and Unit 2 Heat Removal System performance indicator for Byron Unit 1
No findings of significance were identified. .3 High Risk Significant, High Dose Rate, High Radiation Area, and Very High Radiation
    and Unit 2 for the period from the fourth quarter 2007 through the third quarter 2008.
Area Controls
    To determine the accuracy of the PI data reported during those periods, PI definitions
a. Inspection Scope
    and guidance contained in the NEI Document 99-02, Regulatory Assessment
The inspectors held discussions with the Radiation Protection Manager concerning high dose rate, high radiation area and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection, in order to assess whether any procedure modifications substantially reduced the effectiveness and level of worker protection. The inspectors discussed with radiation protection supervisors the controls that were in place for special areas of the plant that had the potential to become very high radiation areas during certain plant operations.  The inspectors assessed if plant operations required communication beforehand with the radiation protection group, so as to allow
    Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the
corresponding timely actions to properly post and control the radiation hazards. 
    licensees operator narrative logs, issue reports, event reports, MSPI derivation reports,
Documents reviewed were listed in the Attachment. 
    and NRC Integrated Inspection Reports for the period of October 2007 through
Enclosure
    September 2008 to validate the accuracy of the submittals. The inspectors reviewed the
22This inspection constitutes one sample as defined in IP 71121.01-5. b. Findings
    MSPI component risk coefficient to determine if it had changed by more than 25 percent
No findings of significance were identified. .4 Radiation Worker Performance
    in value since the previous inspection, and if so, that the change was in accordance with
a. Inspection Scope
    applicable NEI guidance. The inspectors also reviewed the licensees issue report
The inspectors reviewed radiological problem reports for which the cause of the event was due to radiation worker errors to determine if there was an observable pattern
    database to determine if any problems had been identified with the PI data collected or
traceable to a similar cause and to determine if this perspective matched the corrective
    transmitted for this indicator and none were identified. Documents reviewed are listed in
action approach taken by the licensee to resolve the reported problems.  Problems or issues with planned or completed corrective actions were discussed with the Radiation Protection Manager.  Documents reviewed were listed in the Attachment. This inspection constitutes one sample as defined in IP 71121.01-5. b. Findings
    the Attachment to this report.
No findings of significance were identified. .5 Radiation Protection Technician Proficiency
    This inspection constituted two MSPI heat removal system samples as defined in
a. Inspection Scope
    IP 71151-05.
The inspectors reviewed radiological problem reports for which the cause of the event was radiation protection technician error to determine if there was an observable pattern
  b. Findings
traceable to a similar cause and to determine if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems.  Documents reviewed were listed in the Attachment.  This inspection constitutes one sample as defined in IP 71121.01-5. b. Findings
    No findings of significance were identified.
No findings of significance were identified.
.4   Mitigating Systems Performance Index - Residual Heat Removal System
2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02) .1 Radiological Work Planning
  a. Inspection Scope
a. Inspection Scope
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
The inspectors evaluated the licensee's list of work activities ranked by estimated exposure that were in progress and reviewed the following two work activities of highest exposure significance: 
    Index - Unit 1 and Unit 2 Residual Heat Removal System performance indicator for
* Cleaning and Eddy Current Testing of the Seal Table; and
    Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third
* Dye Penetrant Testing of Reactor Head Penetration 68.
    quarter 2008. To determine the accuracy of the PI data reported during those periods,
    
    PI definitions and guidance contained in the NEI Document 99-02, Regulatory
Enclosure
    Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors
23This inspection supplements the sample reported in Inspection Report 05000454/2008002; 05000455/2008002. For these two activities, the inspectors reviewed the ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements in order to verify that the licensee had established procedures and engineering and work controls that were based
    reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports,
on sound radiation protection principles in order to achieve occupational exposures that
    event reports, and NRC Integrated Inspection Reports for the period of October 2007
were ALARA.  The inspectors also determined if the licensee had reasonably grouped
    through September 2008 to validate the accuracy of the submittals. The inspectors
the radiological work into work activities, based on historical precedence, industry
    reviewed the MSPI component risk coefficient to determine if it had changed by more
norms, and/or special circumstances.  This inspection supplements the sample reported in Inspection Report 05000454/2008002; 05000455/2008002. Documents reviewed were listed in the Attachment. b. Findings
    than 25 percent in value since the previous inspection, and if so, that the change was in
No findings of significance were identified. .2 Radiation Worker Performance
    accordance with applicable NEI guidance. The inspectors also reviewed the licensees
a. Inspection Scope
    issue report database to determine if any problems had been identified with the PI data
Radiation worker and radiation protection technician performance was observed during work activities being performed in radiation areas, airborne radioactivity areas, and high
    collected or transmitted for this indicator and none were identified. Documents reviewed
radiation areas that presented the greatest radiological risk to workers.  The inspectors
    are listed in the Attachment to this report.
evaluated whether workers demonstrated the ALARA philosophy by being familiar with the scope of the work activity and tools to be used, by utilizing ALARA low dose waiting
    This inspection constituted two MSPI residual heat removal system samples as defined
areas, and by complying with work activity controls.  Also, radiation worker training and
    in IP 71151-05.
skill levels were reviewed to determine if they were sufficient relative to the radiological hazards and the work involved.  Documents reviewed were listed in the Attachment. This inspection supplements the sample reported in Inspection Report 05000454/2008002; 05000455/2008002. b. Findings
                                              25                                     Enclosure
No findings of significance were identified.
4OA1 Performance Indicator Verification (71151) .1 Mitigating Systems Performance
Index - Emergency AC Power System
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - Unit 1 and Unit 2 Emergency AC Power System performance indicator
for Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third
quarter 2008.  To determine the accuracy of the Performance Indicators (PI) data reported during those periods, PI definitions and guidance contained in the Nuclear 
Enclosure
24Energy Institute (NEI) Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used.  The inspectors reviewed the licensee's operator
narrative logs, MSPI derivation reports, issue reports, event reports, and NRC Integrated Inspection Reports for the period of October 2007 through September 2008 to validate the accuracy of the submittals.  The inspectors reviewed the MSPI component risk
coefficient to determine if it had changed by more than 25 percent in value since the
previous inspection, and if so, that the change was in accordance with applicable
NEI guidance.  The inspectors also reviewed the licensee's issue report database to
determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.  Documents reviewed are listed in the Attachment to this report. This inspection constituted two MSPI emergency AC power system samples as defined
in IP 71151-05. b. Findings
No findings of significance were identified. .2 Mitigating Systems Performance Index - High Pressure Injection Systems
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Unit 1 and Unit 2 High Pressure Injection Systems performance indicator for Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third quarter 2008.  To determine the accuracy of the PI data reported during those periods,
PI definitions and guidance contained in the NEI Document 99-02, "Regulatory
Assessment Performance Indicator Guideline," Revision 5, were used.  The inspectors
reviewed the licensee's operator narrative l
ogs, issue reports, MSPI derivation reports, event reports, and NRC Integrated Inspection Reports for the period of October 2007 to September 2008 to validate the accuracy of the submittals.  The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent
in value since the previous inspection, and if so, that the change was in accordance with
applicable NEI guidance.  The inspectors also reviewed the licensee's issue report
database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.  Documents reviewed are listed in the Attachment to this report. This inspection constituted two MSPI high pressure injection system samples as defined
in IP 71151-05. b. Findings
No findings of significance were identified. 
Enclosure
25.3 Mitigating Systems Performance Index - Heat Removal System
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Unit 1 and Unit 2 Heat Removal System performance indicator for Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third quarter 2008.  
To determine the accuracy of the PI data reported during those periods, PI definitions  
and guidance contained in the NEI Document 99-02, "Regulatory Assessment  
Performance Indicator Guideline," Revision 5, were used. The inspectors reviewed the  
licensee's operator narrative logs, issue reports, event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the period of October 2007 through September 2008 to validate the accuracy of the submittals. The inspectors reviewed the  
MSPI component risk coefficient to determine if it had changed by more than 25 percent  
in value since the previous inspection, and if so, that the change was in accordance with  
applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in  
the Attachment to this report. This inspection constituted two MSPI heat removal system samples as defined in  
IP 71151-05. b. Findings
No findings of significance were identified. .4 Mitigating Systems Performance Index - Residual Heat Removal System
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Unit 1 and Unit 2 Residual Heat Removal System performance indicator for Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third quarter 2008. To determine the accuracy of the PI data reported during those periods,  
PI definitions and guidance contained in the NEI Document 99-02, "Regulatory  
Assessment Performance Indicator Guideline," Revision 5, were used. The inspectors  
reviewed the licensee's operator narrative l
ogs, issue reports, MSPI derivation reports, event reports, and NRC Integrated Inspection Reports for the period of October 2007 through September 2008 to validate the accuracy of the submittals. The inspectors  
reviewed the MSPI component risk coefficient to determine if it had changed by more  
than 25 percent in value since the previous inspection, and if so, that the change was in  
accordance with applicable NEI guidance. The inspectors also reviewed the licensee's
issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. This inspection constituted two MSPI residual heat removal system samples as defined  
in IP 71151-05.
Enclosure
26b. Findings
No findings of significance were identified. .5 Mitigating Systems Performanc
e Index - Cooling Water Systems
a. Inspection Scope
The inspectors sampled licensee submittals for the Unit 1 and Unit 2 Mitigating Systems Performance Index - Unit 1 and Unit 2 Cooling Water Systems performance indicator for
Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third
quarter 2008.  To determine the accuracy of the PI data reported during those periods,
PI definitions and guidance contained in the NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used.  The inspectors reviewed the licensee's operator narrative l
ogs, issue reports, MSPI derivation reports, event reports, and NRC Integrated Inspection Reports for the period of October 2007
through September 2008 to validate the accuracy of the submittals.  The inspectors
reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance.  The inspectors also reviewed the licensee's
issue report database to determine if any problems had been identified with the PI data
collected or transmitted for this indicator and none were identified.  Documents reviewed
are listed in the Attachment to this report. This inspection constituted two MSPI cooling water system samples as defined in
IP 71151-05. b. Findings
No findings of significance were identified. .6 Reactor Coolant System Specific Activity
a. Inspection Scope
The inspectors sampled licensee submittals for the Reactor Coolant System (RCS) Specific Activity performance indicator for the period of June 2007 through August 2008
to determine the accuracy of the PI data reported during those periods, PI definitions
and guidance contained in the NEI Document 99-02, "Regulatory Assessment
Performance Indicator Guideline," Revision 5, were used.  The inspectors reviewed the licensee's RCS chemistry samples, TS requirements, issue reports, event reports and NRC Integrated Inspection Reports for the period of June 2007 through August 2008 to
validate the accuracy of the submittals.  The inspectors also reviewed the licensee's
issue report database to determine if any problems had been identified with the PI data
collected or transmitted for this indicator and none were identified.  In addition to record
reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample.  Documents reviewed are listed in the Attachment to this report. This inspection constituted two reactor coolant system specific activity samples as defined in IP 71151-05. 
Enclosure  
27b. Findings
No findings of significance were identified. .7 Reactor Coolant System Leakage
a. Inspection Scope
The inspectors sampled licensee submittals for the RCS Leakage performance indicator
Unit 1 Reactor Coolant System Identified Leakage and Unit 2 Reactor Coolant System Identified Leakage.  To determine the accuracy of the PI data reported during those
periods, PI definitions and guidance contained in the NEI Document 99-02, "Regulatory
Assessment Performance Indicator Guideline," Revision 5, were used.  The inspectors reviewed the licensee's operator logs, RCS leakage tracking data, issue reports, event reports, and NRC Integrated Inspection Reports for the period of March 2007 to
November 2008 to validate the accuracy of the submittals.  The inspectors also reviewed
the licensee's issue report database to determine if any problems had been identified
with the PI data collected or transmitted for this indicator and none were identified.  Documents reviewed are listed in the Attachment to this report. This inspection constituted two reactor coolant system leakage samples as defined in
IP 71151-05. b. Findings
No findings of significance were identified. .8 Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent
Occurrences
a. Inspection Scope
The inspectors sampled licensee submittals for the Radiological Effluent TS (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences
performance indicator for the period of June 2007 through August 2008.  The inspectors used PI definitions and guidance contained in the NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5 to determine the accuracy of
the PI data reported during those periods.  The inspectors reviewed the licensee's issue
report database and selected individual reports generated since this indicator was last
reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose.  The inspectors reviewed gaseous effluent summary data and the results of associated offsite
dose calculations for selected dates between June 2007 and August 2008 to determine
if indicator results were accurately reported.  The inspectors also reviewed the licensee's
methods for quantifying gaseous and liquid effluents and determining effluent dose. 
Documents reviewed are listed in the Attachment to this report. This inspection constituted one RETS/ODCM radiological effluent occurrences sample
as defined in IP 71151-05. 
Enclosure
28b. Findings
No findings of significance were identified. 4OA2 Identification and Resolution of Problems (71152) Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
Physical Protection .1 Routine Review of items Entered Into the Corrective Action Program
a. Inspection Scope
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's CAP at
an appropriate threshold, that adequate attention was being given to timely corrective
actions, and that adverse trends were identified and addressed.  Attributes reviewed
included:  the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root
causes, extent of condition reviews, and previous occurrences reviews were proper and
adequate; and that the classification, prioritization, focus, and timeliness of corrective
actions were commensurate with safety and sufficient to prevent recurrence of the issue.  Minor issues entered into the licensee's CAP as a result of the inspectors' observations are included in the attached List of Documents Reviewed. These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples.  Instead, by procedure they were considered an
integral part of the inspections performed during the quarter and documented in
Section 1 of this report. b. Findings
No findings of significance were identified. .2 Daily Corrective Action Program Reviews
a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's CAP.  This review was accomplished through
inspection of the station's daily condition report packages. These daily reviews were performed by procedure as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples. 
Enclosure
29b. Findings
No findings of significance were identified. .3 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue.  The
inspectors' review was focused on repetitive equipment issues, but also considered the
results of daily inspector CAP item screening discussed in Section 4OA2.2 above, licensee trending efforts, and licensee human performance results.  The inspectors' review nominally considered the 6 month per
iod of July 01 through December 31, 2008, although some examples expanded beyond those dates when the scope of the trend


warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments.  The inspectors
  b. Findings
compared and contrasted their results with the results contained in the licensee's
    No findings of significance were identified.
CAP trending reports.  Corrective actions associated with a sample of the issues
.5  Mitigating Systems Performance Index - Cooling Water Systems
identified in the licensee's trending reports were reviewed for adequacy. This review constituted a single semi-annual trend inspection sample as defined in
  a. Inspection Scope
IP 71152-05. b. Findings
    The inspectors sampled licensee submittals for the Unit 1 and Unit 2 Mitigating Systems
No findings of significance were identified. .4 Selected Issue Follow-Up Inspection:  Byron Review of Potential Preconditioning Issue
    Performance Index - Unit 1 and Unit 2 Cooling Water Systems performance indicator for
a. Inspection Scope
    Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third
During a review of items entered in the licensee's CAP, the inspectors observed that the licensee was following up on potential preconditioning issues identified at Braidwood for  
    quarter 2008. To determine the accuracy of the PI data reported during those periods,
applicability to Byron Station.  The inspectors selected this issue for a follow-up
    PI definitions and guidance contained in the NEI Document 99-02, Regulatory
inspection on problem identification and resolution.  Documents reviewed are listed in
    Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors
the Attachment to this report. This review constituted one in-depth problem identification and resolution sample as defined in IP 71152-05. b. Findings and Observations
    reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports,
In October 2007, the licensee at Braidwood identified a number of potential preconditioning issues of motor-operated and air-operated valves.  Specifically,
    event reports, and NRC Integrated Inspection Reports for the period of October 2007
preventive maintenance tasks were being performed on the valves prior to the inservice test such that testing was not being conducted in the as-found condition. Although the 
    through September 2008 to validate the accuracy of the submittals. The inspectors
Enclosure
    reviewed the MSPI component risk coefficient to determine if it had changed by more
30ASME Code does not specifically require as-found testing, the NRC had issued several generic communications on the subject to ensure licensees evaluated the potential
    than 25 percent in value since the previous inspection, and if so, that the change was in
affects of the maintenance on the test results.  An action request was initiated to review this issue for applicability to Byron. In December 2007, the licensee's corporate support group, the licensee and its sister
    accordance with applicable NEI guidance. The inspectors also reviewed the licensees
sites discussed this issue and developed draft guidance on preconditioning.  One area that was considered to be potentially preconditioning was performing stem lubrications on a valve on the same frequency as the inservice test. In February 2008, in advance of refueling outage B1R15, the licensee conducted a review of valves that were tested on a cold shutdown or refueling outage frequency. The review was performed to determine whether any preventive maintenance was going to
    issue report database to determine if any problems had been identified with the PI data
be performed prior to the inservice test on the valve, which could be presumed to be
    collected or transmitted for this indicator and none were identified. Documents reviewed
preconditioning.  This review did not identify any instances of preconditioning.  The
    are listed in the Attachment to this report.
inspectors, however, questioned six valves that had stem lubrication frequency of once a refueling cycle and appeared to be performed on the valves prior to the test.  This did not appear to meet the licensee's guidance in Procedure ER-AA-302-1006, "Generic
    This inspection constituted two MSPI cooling water system samples as defined in
Letter 96-05 Program Motor-Operated Valve Maintenance and Testing Guidelines," or
    IP 71151-05.
the newly developed draft guidance for what could be potentially considered
  b. Findings
preconditioning. The guidance stated that stem lubrication would not be considered preconditioning unless it was routinely scheduled immediately before and at the same frequency as the valve test.  These six valves appeared to meet the guidance for being
    No findings of significance were identified.
potentially preconditioning issues. Although the inspectors determined that these valves should have been flagged in the action request as having potential preconditioning concerns, further review by the  
.6  Reactor Coolant System Specific Activity
licensee indicated that with the exception of one valve, all the stem lubrications were performed after the inservice test during the outage. The one exception also had several other maintenance activities performed during the outage and it was not
  a. Inspection Scope
conclusive if the testing was performed prior to or after the maintenance.  The licensee
    The inspectors sampled licensee submittals for the Reactor Coolant System (RCS)
indicated that there was not any guidance with respect to the schedule as to whether
    Specific Activity performance indicator for the period of June 2007 through August 2008
testing or maintenance should be performed first. The issue of preconditioning of motor-operated valves prior to their diagnostic test to meet Generic Letter 96-05, "Periodic Verification of Design-Basis Capability of Safety-Related Power-Operated Valves," may
    to determine the accuracy of the PI data reported during those periods, PI definitions
also be an issue as it may not be possible to verify the valve would have been capable to operate under design basis conditions for the time frame since the last maintenance
    and guidance contained in the NEI Document 99-02, Regulatory Assessment
or test without the as-found testing. Although no specific preconditioning issues were
    Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the
identified, additional scheduling guidance or training may be warranted to highlight the potential for preconditioning by not testing valves in their as-found condition. No findings of significance were identified. .5 4OA5 Other Activities Implementation of Temporary Instruction (TI) 2515/176, "Emergency Diesel Generator Technical Specification Surveillance Requirements Regarding Endurance and Margin Testing"
    licensees RCS chemistry samples, TS requirements, issue reports, event reports and
a. Inspection Scope
    NRC Integrated Inspection Reports for the period of June 2007 through August 2008 to
The objective of TI 2515/176 was to gather information to assess the adequacy of nuclear power plant emergency diesel generator endurance and margin testing as
    validate the accuracy of the submittals. The inspectors also reviewed the licensees
prescribed in plant-specific TS. The inspectors reviewed the licensee's TS, procedures,
    issue report database to determine if any problems had been identified with the PI data
Enclosure
    collected or transmitted for this indicator and none were identified. In addition to record
31and calculations, and interviewed licensee personnel to complete the TI. The information gathered for this TI was forwarded to the Office of Nuclear Reactor
    reviews, the inspectors observed a chemistry technician obtain and analyze a reactor
Regulation for further review and evaluation on December 17, 2008.  This TI is complete at Byron Station; however, this TI 2515/176 will not expire until August 31, 2009.  Additional information may be required after review by the Office of Nuclear Reactor
    coolant system sample. Documents reviewed are listed in the Attachment to this report.
Regulation. b. Findings
    This inspection constituted two reactor coolant system specific activity samples as
No findings of significance were identified. .6 Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review
    defined in IP 71151-05.
a. Inspection Scope
                                              26                                      Enclosure
The inspectors reviewed the final report for the INPO plant assessment conducted in June 2008 and dated December 2008. The inspectors reviewed the report to ensure


that issues identified were consistent
  b. Findings
with the NRC perspectives of licensee performance and to verify if any significant safety issues were identified that required
      No findings of significance were identified.
further NRC follow-up. b. Findings
.7   Reactor Coolant System Leakage
No findings of significance were identified. .7 Quarterly Resident Inspector Observations of Security Personnel and Activities
  a. Inspection Scope
a. Inspection Scope
      The inspectors sampled licensee submittals for the RCS Leakage performance indicator
During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. 
      Unit 1 Reactor Coolant System Identified Leakage and Unit 2 Reactor Coolant System
These observations took place during both normal and off-normal plant working hours.  
      Identified Leakage. To determine the accuracy of the PI data reported during those
* Multiple tours of operations within the Central and Secondary Security Alarm
      periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
Stations;
      Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors
* Owner Controlled Area and Protected Area access control posts;
      reviewed the licensees operator logs, RCS leakage tracking data, issue reports, event
* Other security officer posts including the ready room and compensatory posts;
      reports, and NRC Integrated Inspection Reports for the period of March 2007 to
and Security equipment log review. The inspectors also reviewed a report of the results of a survey of the site security organization relative to its safety conscious work environment.  The inspectors
      November 2008 to validate the accuracy of the submittals. The inspectors also reviewed
considered whether the surveys were conducted in a manner that encouraged candid and honest feedback.  The results were reviewed to determine whether an adequate number of staff responded to the survey. The inspectors also reviewed Exelon's self-assessment of the survey results and verified that any issues or areas for improvement were entered into the corrective action program for resolution. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities.  
      the licensees issue report database to determine if any problems had been identified
  Enclosure
      with the PI data collected or transmitted for this indicator and none were identified.
32b. Findings
      Documents reviewed are listed in the Attachment to this report.
No findings of significance were identified. .8 (Closed) Unresolved Items (URI) 05000454/455/2008003-06:  Auxiliary Feedwater
      This inspection constituted two reactor coolant system leakage samples as defined in
Tunnel Hatch Margin to Safety
      IP 71151-05.
The licensee had identified that the design analysis for evaluation of the Auxiliary Feedwater (AFW) tunnel flood seal covers did not include the effects of a high energy
  b.  Findings
      No findings of significance were identified.
.8   Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent
      Occurrences
  a.  Inspection Scope
      The inspectors sampled licensee submittals for the Radiological Effluent TS
      (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences
      performance indicator for the period of June 2007 through August 2008. The inspectors
      used PI definitions and guidance contained in the NEI Document 99-02, Regulatory
      Assessment Performance Indicator Guideline, Revision 5 to determine the accuracy of
      the PI data reported during those periods. The inspectors reviewed the licensees issue
      report database and selected individual reports generated since this indicator was last
      reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or
      improperly calculated effluent releases that may have impacted offsite dose. The
      inspectors reviewed gaseous effluent summary data and the results of associated offsite
      dose calculations for selected dates between June 2007 and August 2008 to determine
      if indicator results were accurately reported. The inspectors also reviewed the licensees
      methods for quantifying gaseous and liquid effluents and determining effluent dose.
      Documents reviewed are listed in the Attachment to this report.
      This inspection constituted one RETS/ODCM radiological effluent occurrences sample
      as defined in IP 71151-05.
                                              27                                        Enclosure


line break in the main steam isolation valve tunnels at another facilityThe NRC inspectors at that facility questioned why a dynamic load factor as a result of the impulse
  b. Findings
pressure following a high energy line break had not been considered in an analytic calculation performed to support the operability evaluation.  Following a review of the licensee's evaluation, the inspectors questioned the licensee's conclusion that the operability of the AFW hatches continued to be supported despite
      No findings of significance were identified.
analytical results showing a factor of safety for the concrete expansion anchors
4OA2 Identification and Resolution of Problems (71152)
supporting the hatches of less than 2.0, which is contrary to the guidance provided in
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
NRC Bulletin 79-02, "Pipe Support Base Plate Designs Using Concrete Expansion Anchors."  Additionally, the inspectors noted that the licensee's evaluation did not  
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
      Physical Protection
  .1  Routine Review of items Entered Into the Corrective Action Program
  a. Inspection Scope
      As part of the various baseline inspection procedures discussed in previous sections of
      this report, the inspectors routinely reviewed issues during baseline inspection activities
      and plant status reviews to verify that they were being entered into the licensees CAP at
      an appropriate threshold, that adequate attention was being given to timely corrective
      actions, and that adverse trends were identified and addressed. Attributes reviewed
      included: the complete and accurate identification of the problem; that timeliness was
      commensurate with the safety significance; that evaluation and disposition of
      performance issues, generic implications, common causes, contributing factors, root
      causes, extent of condition reviews, and previous occurrences reviews were proper and
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
      Minor issues entered into the licensees CAP as a result of the inspectors observations
      are included in the attached List of Documents Reviewed.
      These routine reviews for the identification and resolution of problems did not constitute
      any additional inspection samples. Instead, by procedure they were considered an
      integral part of the inspections performed during the quarter and documented in
      Section 1 of this report.
  b. Findings
      No findings of significance were identified.
.2   Daily Corrective Action Program Reviews
  a. Inspection Scope
      In order to assist with the identification of repetitive equipment failures and specific
      human performance issues for follow-up, the inspectors performed a daily screening of
      items entered into the licensees CAP. This review was accomplished through
      inspection of the stations daily condition report packages.
      These daily reviews were performed by procedure as part of the inspectors daily plant
      status monitoring activities and, as such, did not constitute any separate inspection
      samples.
                                                28                                      Enclosure


address Section C.13 of NRC Technical Guidance 9900, "Operability Determinations &
  b. Findings
Functionality Assessment for Resolution of Degraded or Nonconforming Conditions
    No findings of significance were identified.
Adverse to Quality or Safety."  Specifically, Section C.13 stated that if a structure was degraded, the licensee should assess the structure's capability of performing its specified function. As long as the identified degradation did not result in exceeding
.3  Semi-Annual Trend Review
acceptance limits specified in applicable design codes and standards referenced in the
  a. Inspection Scope
design basis documents, the affected structure was either operable or functional. The  
    The inspectors performed a review of the licensees CAP and associated documents to
licensee also identified additional errors that reduced the margin of safety for the
    identify trends that could indicate the existence of a more significant safety issue. The
structural integrity of a high energy line break barrier.  At the close of the inspection period that opened this URI, temporary modifications were implemented at both facilities that restored the margin of safety to greater than 2.0. 
    inspectors review was focused on repetitive equipment issues, but also considered the
Pending additional follow-up by the inspectors for the past operability and timeliness of
    results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
corrective actions, extent of condition, and corrective actions, a URI was opened. During this inspection period, the issue was assessed by regional inspectors at the other facility.  The inspectors' conclusions were reviewed by the inspectors at Byron and confirmed to be applicable to Byron. The inspectors documented their review in  
    licensee trending efforts, and licensee human performance results. The inspectors
Section 4OA7 as two licensee-identified violations. This URI is closed. 4OA6  Management Meetings
    review nominally considered the 6 month period of July 01 through December 31, 2008,
.1 Exit Meeting Summary
    although some examples expanded beyond those dates when the scope of the trend
On January 15, 2009, the inspectors presented the inspection results to Mr. D. Hoots and other members of the licensee staff.  The licensee acknowledged the issues presented.  The inspectors confirmed that none of the material examined during the  
    warranted.
inspection was proprietary. .2 Interim Exit Meetings
    The review also included issues documented outside the normal CAP in major
 
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
Enclosure
    problem/challenges lists, system health reports, quality assurance audit/surveillance
33 Interim exits were conducted for:
    reports, self assessment reports, and Maintenance Rule assessments. The inspectors
* Occupational Radiation Safety Program for Access to Radiologically Significant Areas and Performance Indicator Verification with Mr. D. Hoots, and other members of the licensee's staff on October 10, 2008.  
    compared and contrasted their results with the results contained in the licensees
* Inservice Inspection 71111.08 with Mr. D. Hoots on October 16, 2008. The inspectors returned proprietary information reviewed during the inspection prior
    CAP trending reports. Corrective actions associated with a sample of the issues
to leaving the site.  
    identified in the licensees trending reports were reviewed for adequacy.
* TI 2515/176 via telephone with Mr. B. Grundmann and other licensee staff on November 25, 2008.
    This review constituted a single semi-annual trend inspection sample as defined in
* The licensed operator requalification training written examination and operating test construction and the biennial written examination and annual operating test results with Mr. G. Wolfe via telephone on December 15, 2008.
    IP 71152-05.
  b. Findings
The inspectors confirmed that none of the potential report input discussed was
    No findings of significance were identified.
.4  Selected Issue Follow-Up Inspection: Byron Review of Potential Preconditioning Issue
  a. Inspection Scope
    During a review of items entered in the licensees CAP, the inspectors observed that the
    licensee was following up on potential preconditioning issues identified at Braidwood for
    applicability to Byron Station. The inspectors selected this issue for a follow-up
    inspection on problem identification and resolution. Documents reviewed are listed in
    the Attachment to this report.
    This review constituted one in-depth problem identification and resolution sample as
    defined in IP 71152-05.
  b. Findings and Observations
    In October 2007, the licensee at Braidwood identified a number of potential
    preconditioning issues of motor-operated and air-operated valves. Specifically,
    preventive maintenance tasks were being performed on the valves prior to the inservice
    test such that testing was not being conducted in the as-found condition. Although the
                                              29                                      Enclosure


considered proprietary.  
    ASME Code does not specifically require as-found testing, the NRC had issued several
    generic communications on the subject to ensure licensees evaluated the potential
    affects of the maintenance on the test results. An action request was initiated to review
    this issue for applicability to Byron.
    In December 2007, the licensees corporate support group, the licensee and its sister
    sites discussed this issue and developed draft guidance on preconditioning. One area
    that was considered to be potentially preconditioning was performing stem lubrications
    on a valve on the same frequency as the inservice test.
    In February 2008, in advance of refueling outage B1R15, the licensee conducted a
    review of valves that were tested on a cold shutdown or refueling outage frequency. The
    review was performed to determine whether any preventive maintenance was going to
    be performed prior to the inservice test on the valve, which could be presumed to be
    preconditioning. This review did not identify any instances of preconditioning. The
    inspectors, however, questioned six valves that had stem lubrication frequency of once a
    refueling cycle and appeared to be performed on the valves prior to the test. This did
    not appear to meet the licensees guidance in Procedure ER-AA-302-1006, Generic
    Letter 96-05 Program Motor-Operated Valve Maintenance and Testing Guidelines, or
    the newly developed draft guidance for what could be potentially considered
    preconditioning. The guidance stated that stem lubrication would not be considered
    preconditioning unless it was routinely scheduled immediately before and at the same
    frequency as the valve test. These six valves appeared to meet the guidance for being
    potentially preconditioning issues.
    Although the inspectors determined that these valves should have been flagged in the
    action request as having potential preconditioning concerns, further review by the
    licensee indicated that with the exception of one valve, all the stem lubrications were
    performed after the inservice test during the outage. The one exception also had
    several other maintenance activities performed during the outage and it was not
    conclusive if the testing was performed prior to or after the maintenance. The licensee
    indicated that there was not any guidance with respect to the schedule as to whether
    testing or maintenance should be performed first. The issue of preconditioning of motor-
    operated valves prior to their diagnostic test to meet Generic Letter 96-05, Periodic
    Verification of Design-Basis Capability of Safety-Related Power-Operated Valves, may
    also be an issue as it may not be possible to verify the valve would have been capable
    to operate under design basis conditions for the time frame since the last maintenance
    or test without the as-found testing. Although no specific preconditioning issues were
    identified, additional scheduling guidance or training may be warranted to highlight the
    potential for preconditioning by not testing valves in their as-found condition.
    No findings of significance were identified.
.5  4OA5 Other Activities Implementation of Temporary Instruction (TI) 2515/176,
    Emergency Diesel Generator Technical Specification Surveillance Requirements
    Regarding Endurance and Margin Testing
  a. Inspection Scope
    The objective of TI 2515/176 was to gather information to assess the adequacy of
    nuclear power plant emergency diesel generator endurance and margin testing as
    prescribed in plant-specific TS. The inspectors reviewed the licensee's TS, procedures,
                                              30                                      Enclosure


4OA7 Licensee-Identified Violations
    and calculations, and interviewed licensee personnel to complete the TI. The
  The following violation of very low significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of Section VI of the NRC
    information gathered for this TI was forwarded to the Office of Nuclear Reactor
Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.  
    Regulation for further review and evaluation on December 17, 2008. This TI is complete
* NRC Order EA-03-009, for Byron Unit 2, requires that t
    at Byron Station; however, this TI 2515/176 will not expire until August 31, 2009.
he licensee perform ultrasonic testing of each RPV head penetration nozzle every refueling outage because of its high susceptibility ranking. Contrary to this, the licensee
    Additional information may be required after review by the Office of Nuclear Reactor
discovered during the current B2R14 outage that penetration 41 was not ultrasonically tested during the prior Unit 2 outage in April 2007 (B2R13). No observable boric acid deposits were noted as a result of the bare metal visual
    Regulation.
examination of the penetration nozzles performed during outages B2R13 and
  b. Findings
B2R14; and there were no reportable indications found as a result of the B2R14
    No findings of significance were identified.
ultrasonic test of penetration 41. Based upon this, the violation was of very low safety significance.  The licensee entered this issue into the corrective action
.6  Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review
program as IR 829647.
  a. Inspection Scope
* 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and
    The inspectors reviewed the final report for the INPO plant assessment conducted in
equipment, and non-conformances are promptly identified and corrected.  Licensee Procedure LS-AA-125, Revision 12, "Corrective Action Program (CAP) Procedure," was written in accordance with Criterion XVI.  Step 2.12 of  
    June 2008 and dated December 2008. The inspectors reviewed the report to ensure
LS-AA-125 requires, in part, "-a Corrective Action is any action that meets any of the following.-  Is necessary to restore a Significance Level 1, 2, or 3
    that issues identified were consistent with the NRC perspectives of licensee
Condition-."  Contrary to the above, on October 22, 2008, licensee personnel
    performance and to verify if any significant safety issues were identified that required
failed to correct a condition adverse to quality as stated in IR 834410. Specifically, loose debris that had been left on the polar crane had not been removed prior to Unit 2 changing from Mode 5 to Mode 4. IR 834410 had been
    further NRC follow-up.
designated by the licensee as a Significance level 3 condition. This issue is of  
  b. Findings
very low safety significance because this finding was not a design or qualification
    No findings of significance were identified.
deficiency, did not result in loss of system or train safety function and was not safety significant due to external events. 
.7  Quarterly Resident Inspector Observations of Security Personnel and Activities
Enclosure
  a. Inspection Scope
34 * 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and
    During the inspection period, the inspectors conducted observations of security force
equipment, and non-conformances are promptly identified and corrected. Contrary to the above, since April 18, 2007, the licensee failed to promptly identify and correct conditions adverse to quality regarding design of AFW tunnel
    personnel and activities to ensure that the activities were consistent with licensee
hatch covers.  Specifically, upon finding a design deficiency in the hatch
    security procedures and regulatory requirements relating to nuclear plant security.
structural calculation, the licensee failed to promptly identify all the related design
    These observations took place during both normal and off-normal plant working hours.
issues through more detailed reviews and field inspections, and to complete
    *        Multiple tours of operations within the Central and Secondary Security Alarm
corrective actions to address the design deficiencies and to restore the design margins. This finding was of very low safety significance because the finding did not represent an actual open pathway in the physical integrity of reactor
              Stations;
containment.  The issue was identified in the licensee's CAP as IR 857487.  The
    *        Owner Controlled Area and Protected Area access control posts;
licensee had completed a temporary modification to increase the safety margin of
    *        Other security officer posts including the ready room and compensatory posts;
the hatches and is in the process of designing a permanent modification to restore full design margin.
              and Security equipment log review.
* 10 CFR Part 50, Appendix B, Criterion III, "Design Control," required, in part, that design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or
    The inspectors also reviewed a report of the results of a survey of the site security
simplified calculation methods, or by the performance of a suitable testing
    organization relative to its safety conscious work environment. The inspectors
program. Contrary to this, on December 4, 1987, the licensee failed to ensure design measures were in place for verifying or checking the adequacy of AFW hatch cover plate design.  Specifically, in Calculation 5.6.3.9, the licensee failed
    considered whether the surveys were conducted in a manner that encouraged candid
to ensure that a safety factor in accordance with the station design criteria was
    and honest feedback. The results were reviewed to determine whether an adequate
applied in the design of expansion anchors.  The issue was identified in the  
    number of staff responded to the survey. The inspectors also reviewed Exelons
licensee's corrective action as IR 654270. This finding was of very low safety
    self-assessment of the survey results and verified that any issues or areas for
significance because it did not represent an actual open pathway in the physical integrity of reactor containment.  
    improvement were entered into the corrective action program for resolution.
    These quarterly resident inspector observations of security force personnel and activities
ATTACHMENT:  SUPPLEMENTAL INFORMATION 
    did not constitute any additional inspection samples. Rather, they were considered an
Attachment
    integral part of the inspectors' normal plant status review and inspection activities.
1SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT
                                                31                                      Enclosure
Licensee D. Hoots, Site Vice President
W. Grundmann, Regulatory Assurance Manager
Z. Cox, Chemist


G. Contrady, Programs Manager
  b. Findings
H. Do, Corporate ISI Engineer
      No findings of significance were identified.
S. Greenlee, Engineering Director D. Thompson, Radiation Protection Manager
.8  (Closed) Unresolved Items (URI) 05000454/455/2008003-06: Auxiliary Feedwater
      Tunnel Hatch Margin to Safety
Nuclear Regulatory Commission
      The licensee had identified that the design analysis for evaluation of the Auxiliary
 
      Feedwater (AFW) tunnel flood seal covers did not include the effects of a high energy
R. Skokowski, Branch Chief
      line break in the main steam isolation valve tunnels at another facility. The NRC
  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
      inspectors at that facility questioned why a dynamic load factor as a result of the impulse
Opened  05000454/2008005-01
      pressure following a high energy line break had not been considered in an analytic
05000455/2008005-01 NCV Failure to Remove or Evaluate Loose Debris Inside of Containment Prior to Applicable Mode
      calculation performed to support the operability evaluation.
05000454/2008005-02
      Following a review of the licensees evaluation, the inspectors questioned the licensees
      conclusion that the operability of the AFW hatches continued to be supported despite
      analytical results showing a factor of safety for the concrete expansion anchors
      supporting the hatches of less than 2.0, which is contrary to the guidance provided in
      NRC Bulletin 79-02, Pipe Support Base Plate Designs Using Concrete Expansion
      Anchors. Additionally, the inspectors noted that the licensees evaluation did not
      address Section C.13 of NRC Technical Guidance 9900, Operability Determinations &
      Functionality Assessment for Resolution of Degraded or Nonconforming Conditions
      Adverse to Quality or Safety. Specifically, Section C.13 stated that if a structure was
      degraded, the licensee should assess the structures capability of performing its
      specified function. As long as the identified degradation did not result in exceeding
      acceptance limits specified in applicable design codes and standards referenced in the
      design basis documents, the affected structure was either operable or functional. The
      licensee also identified additional errors that reduced the margin of safety for the
      structural integrity of a high energy line break barrier.
      At the close of the inspection period that opened this URI, temporary modifications were
      implemented at both facilities that restored the margin of safety to greater than 2.0.
      Pending additional follow-up by the inspectors for the past operability and timeliness of
      corrective actions, extent of condition, and corrective actions, a URI was opened.
      During this inspection period, the issue was assessed by regional inspectors at the other
      facility. The inspectors conclusions were reviewed by the inspectors at Byron and
      confirmed to be applicable to Byron. The inspectors documented their review in
      Section 4OA7 as two licensee-identified violations. This URI is closed.
4OA6 Management Meetings
.1  Exit Meeting Summary
      On January 15, 2009, the inspectors presented the inspection results to Mr. D. Hoots
      and other members of the licensee staff. The licensee acknowledged the issues
      presented. The inspectors confirmed that none of the material examined during the
      inspection was proprietary.
.2  Interim Exit Meetings
                                                32                                      Enclosure


05000455/2008005-02  NCV Failure to Evaluate Radiological Hazards for Airborne
    Interim exits were conducted for:
Radioactivity
    *      Occupational Radiation Safety Program for Access to Radiologically Significant
            Areas and Performance Indicator Verification with Mr. D. Hoots, and other
Closed  05000454/2008005-01
            members of the licensees staff on October 10, 2008.
05000455/2008005-01 NCV Failure to Remove or Evaluate Loose Debris Inside of Containment Prior to Applicable Mode
    *      Inservice Inspection 71111.08 with Mr. D. Hoots on October 16, 2008. The
05000454/2008005-02
            inspectors returned proprietary information reviewed during the inspection prior
            to leaving the site.
    *      TI 2515/176 via telephone with Mr. B. Grundmann and other licensee staff on
            November 25, 2008.
    *      The licensed operator requalification training written examination and operating
            test construction and the biennial written examination and annual operating test
            results with Mr. G. Wolfe via telephone on December 15, 2008.
    The inspectors confirmed that none of the potential report input discussed was
    considered proprietary.
4OA7 Licensee-Identified Violations
    The following violation of very low significance (Green) was identified by the licensee
    and is a violation of NRC requirements which meet the criteria of Section VI of the NRC
    Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
    *      NRC Order EA-03-009, for Byron Unit 2, requires that the licensee perform
            ultrasonic testing of each RPV head penetration nozzle every refueling outage
            because of its high susceptibility ranking. Contrary to this, the licensee
            discovered during the current B2R14 outage that penetration 41 was not
            ultrasonically tested during the prior Unit 2 outage in April 2007 (B2R13). No
            observable boric acid deposits were noted as a result of the bare metal visual
            examination of the penetration nozzles performed during outages B2R13 and
            B2R14; and there were no reportable indications found as a result of the B2R14
            ultrasonic test of penetration 41. Based upon this, the violation was of very low
            safety significance. The licensee entered this issue into the corrective action
            program as IR 829647.
    *      10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part,
            that measures shall be established to assure that conditions adverse to quality,
            such as failures, malfunctions, deficiencies, deviations, defective material and
            equipment, and non-conformances are promptly identified and corrected.
            Licensee Procedure LS-AA-125, Revision 12, Corrective Action Program (CAP)
            Procedure, was written in accordance with Criterion XVI. Step 2.12 of
            LS-AA-125 requires, in part, a Corrective Action is any action that meets any
            of the following. Is necessary to restore a Significance Level 1, 2, or 3
            Condition. Contrary to the above, on October 22, 2008, licensee personnel
            failed to correct a condition adverse to quality as stated in IR 834410.
            Specifically, loose debris that had been left on the polar crane had not been
            removed prior to Unit 2 changing from Mode 5 to Mode 4. IR 834410 had been
            designated by the licensee as a Significance level 3 condition. This issue is of
            very low safety significance because this finding was not a design or qualification
            deficiency, did not result in loss of system or train safety function and was not
            safety significant due to external events.
                                                33                                      Enclosure


05000455/2008005-02 NCV Failure to Evaluate Radiological Hazards for Airborne
    *    10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part,
Radioactivity
          that measures shall be established to assure that conditions adverse to quality,
05000454;
          such as failures, malfunctions, deficiencies, deviations, defective material and
          equipment, and non-conformances are promptly identified and corrected.
          Contrary to the above, since April 18, 2007, the licensee failed to promptly
          identify and correct conditions adverse to quality regarding design of AFW tunnel
          hatch covers. Specifically, upon finding a design deficiency in the hatch
          structural calculation, the licensee failed to promptly identify all the related design
          issues through more detailed reviews and field inspections, and to complete
          corrective actions to address the design deficiencies and to restore the design
          margins. This finding was of very low safety significance because the finding did
          not represent an actual open pathway in the physical integrity of reactor
          containment. The issue was identified in the licensees CAP as IR 857487. The
          licensee had completed a temporary modification to increase the safety margin of
          the hatches and is in the process of designing a permanent modification to
          restore full design margin.
    *    10 CFR Part 50, Appendix B, Criterion III, Design Control, required, in part, that
          design control measures shall provide for verifying or checking the adequacy of
          design, such as by the performance of design reviews, by the use of alternate or
          simplified calculation methods, or by the performance of a suitable testing
          program. Contrary to this, on December 4, 1987, the licensee failed to ensure
          design measures were in place for verifying or checking the adequacy of AFW
          hatch cover plate design. Specifically, in Calculation 5.6.3.9, the licensee failed
          to ensure that a safety factor in accordance with the station design criteria was
          applied in the design of expansion anchors. The issue was identified in the
          licensees corrective action as IR 654270. This finding was of very low safety
          significance because it did not represent an actual open pathway in the physical
          integrity of reactor containment.
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                            34                                        Enclosure


455/2008-003-06 URI Unit 1 and Unit 2 Auxiliary Feedwater Tunnel Hatch Margin  
                              SUPPLEMENTAL INFORMATION
to Safety  
                                KEY POINTS OF CONTACT
Licensee
D. Hoots, Site Vice President
W. Grundmann, Regulatory Assurance Manager
Z. Cox, Chemist
G. Contrady, Programs Manager
H. Do, Corporate ISI Engineer
S. Greenlee, Engineering Director
D. Thompson, Radiation Protection Manager
Nuclear Regulatory Commission
R. Skokowski, Branch Chief
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
05000454/2008005-01      NCV    Failure to Remove or Evaluate Loose Debris Inside of
05000455/2008005-01              Containment Prior to Applicable Mode
05000454/2008005-02      NCV    Failure to Evaluate Radiological Hazards for Airborne
05000455/2008005-02              Radioactivity
Closed
05000454/2008005-01      NCV    Failure to Remove or Evaluate Loose Debris Inside of
05000455/2008005-01              Containment Prior to Applicable Mode
05000454/2008005-02      NCV    Failure to Evaluate Radiological Hazards for Airborne
05000455/2008005-02              Radioactivity
05000454;                URI     Unit 1 and Unit 2 Auxiliary Feedwater Tunnel Hatch Margin
455/2008-003-06                  to Safety
                                                1                                    Attachment


 
                                  LIST OF DOCUMENTS REVIEWED
 
The following is a list of documents reviewed during the inspection. Inclusion on this list does
Attachment
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
2LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection. Inclusion on this list does  
selected sections of portions of the documents were evaluated as part of the overall inspection
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.  
any part of it, unless this is stated in the body of the inspection report.
Section 1R01: Adverse Weather Protection
Section 1R01: Adverse Weather Protection
WO 1020141 01; 89-13 Heat Exchanger Inspection for 2B Diesel Driven AF Pump Closed Cycle  
WO 1020141 01; 89-13 Heat Exchanger Inspection for 2B Diesel Driven AF Pump Closed Cycle
Cooler, October 16, 2008 Issue 846625; Procedure Enhancement, November 18, 2008 BOP SX-T2; SX Tower Operations Guidelines, Revision 12  
Cooler, October 16, 2008
 
Issue 846625; Procedure Enhancement, November 18, 2008
Section 1R04: Equipment Alignment (Quarterly)
BOP SX-T2; SX Tower Operations Guidelines, Revision 12
2BOSR 7.8.1-1; Unit 2 Essential Service Water System Valve Position Monthly Surveillance, Revision 16 BOP DG-1; Diesel Generator Alignment to Standby Condition, Revision 11  
Section 1R04: Equipment Alignment (Quarterly)
BOP VD-5; DG Room Ventilation System Operation, Revision 6  
2BOSR 7.8.1-1; Unit 2 Essential Service Water System Valve Position Monthly Surveillance,
BwOP VD-5; DG Room Ventilation System operation, Revision 12  
Revision 16
BwOS VD-1a; Diesel Ventilation Systems; Revision 4 10 CFR 50.59 Screening, BOP Vd-5 DG Room Ventilation System Operation; January 06, 1986  
BOP DG-1; Diesel Generator Alignment to Standby Condition, Revision 11
BOP VD-5; DG Room Ventilation System Operation, Revision 6
BwOP VD-5; DG Room Ventilation System operation, Revision 12
BwOS VD-1a; Diesel Ventilation Systems; Revision 4
10 CFR 50.59 Screening, BOP Vd-5 DG Room Ventilation System Operation; January 06, 1986
Corrective Action Documents as a Result of NRC Inspection
IR 852537; Compensatory Actions Not Procedurally Directed, December 4, 2008
Section 1R05: Fire Protection (Quarterly)
Corrective Action Documents as a Result of NRC Inspection
Corrective Action Documents as a Result of NRC Inspection
IR 852537; Compensatory Actions Not Procedurally Directed, December 4, 2008 Section 1R05: Fire Protection (Quarterly)
IR 842026; Fire Zone Walkdown Issues, November 07, 2008
Corrective Action Documents as a Result of NRC Inspection
IR 850920; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 842026; Fire Zone Walkdown Issues, November 07, 2008 IR 850920; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008  
IR 850922; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850922; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008  
IR 850925; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850925; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008  
IR 850926; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850926; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008 IR 850929; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008 IR 850931; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008  
IR 850929; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 850932; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008  
IR 850931; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 842026; Fire Zone Walkdown Issues, November 07, 2008  
IR 850932; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
IR 847572; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008  
IR 842026; Fire Zone Walkdown Issues, November 07, 2008
 
IR 847572; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008
Section 1R05: Fire Protection (Annual)
Section 1R05: Fire Protection (Annual)
BAP 1100-10; Response Procedure for Fire, Revision 7 BAP 1100-10T1; 401' Fire Brigade Equipment Inventory, Revision 7  
BAP 1100-10; Response Procedure for Fire, Revision 7
Byron Emergency Self-Contained Breathing Apparatus Storage Locations Monthly Inventory,  
BAP 1100-10T1; 401 Fire Brigade Equipment Inventory, Revision 7
September 2008  
Byron Emergency Self-Contained Breathing Apparatus Storage Locations Monthly Inventory,
OP-AA-201-003; Fire Drill Performance, Revision 7
September 2008
Attachment  
OP-AA-201-003; Fire Drill Performance, Revision 7
3 OP-AA-201-005; Fire Brigade Qualification, Revision 6
                                                    2                                  Attachment
OP-AA-201-008; Pre-Fire Plans, Revision 1
RP-BY-1000; Maintenance Care and Inspection of the ISI Viking Self-Contained Breathing Apparatus (SCBA), Revision 9 Self-Contained Breathing Apparatus Monthly Inspection, September 2008
Byron Station Fire Drill Critique Form, August 24, 2008
Summary Report for Each Shift Reflecting Fire Brigade and HazMat Qualification Status,
October 12, 2008
IR 823253; Safe-Guards Information Slows Fire Response, September 27, 2008
Section 1R07: Heat Sink Performance
WO 1036955; Perform As-Found/As-Left Inspections of 2C RCFC Issue 830146; Replace RCFC Channel Heads with stainless Steel in B2R15, October 13, 2008
IR 830370; Restricted Tubes in 2C RCFC, Need to Plug, October 13, 2008 IR 829315; 2C RCFC Channel Head Degradation, Divider Plates, October 10, 2008
Section 1R08: Inservice Inspection Activities
  IR 829647; Penetration 41 Not Examined During B2R13; October 11, 2008 IR 831084; Foreign Objects Found In 2C SG Secondary Side - B2R14; October 15, 2008 IR 829610; Acceptance Criteria Used On SX Pipe Was Not Appropriate; October 11, 2008
IR 843635, Steam Generator Tube Sheet Inspection Results - B2R14, November 11, 2008
IR 832181; Foreign Objects Found In 2A SG Secondary - B2R14; dated October 17, 2008
IR 830452; B2R14 - Weld Defects Revealed During Radiography Of Repair;  October 14, 2008
IT00717275-02; Buildup of Deposits in Steam Generators, NRC IN 2007-37 ER-AP-335-1012; Bare Metal Visual Examination of PWR Vessel Penetration and Nozzle Safe-
Ends; Revision 3
ER-AP-335-040; Evaluation of Eddy Current Data for Steam Generator Tubing; Revision 4
EXE-ISI-11; Liquid Penetrant Examination, Revision 4
EXE-UT-350; Procedure for Acquiring Material Thickness and Weld Contours; Revision 2 EXE-PDI-UT-2; Ultrasonic Examination of Austenitic Piping Welds in Accordance with PDI-UT-
2; Revision 5
EXAE-ISI-8; VT-1 Direct; Revision 1
ER-AP-335-039; Multi-Frequency Eddy Current Data Acquisition of Steam Generator Tubing;
 
Revision 5
ER-MW-335-1009; Site Specific Performance; Revision 4 ER-AP-331; Boric Acid Corrosion Control (BACC) Program; Revision 3 ER-AP-331-1001; Boric Acid Corrosion control (BACC) Inspection Locations, Implementation
and Inspection Guidelines; Revision 3
ER-AP-331-1002; Boric Acid Corrosion control Program Identification, Screening, and


Evaluation; Revision 4 ER-AP-331-1004; Boric Acid Corrosion Control (BACC) Training and Qualification, Revision 2 ER-AP-420-002; Byron/Braidwood Unit 2: Steam Generator Eddy Current Activities; Revision 8  
OP-AA-201-005; Fire Brigade Qualification, Revision 6
Section 1R11: Licensed Operator Requalification Program
OP-AA-201-008; Pre-Fire Plans, Revision 1
  Six Reactor Operator Biennial Written Examinations for CY 2008; no dates Thirty Senior Reactor Operator Examination Questions for CY 2008 Exams; no dates Twelve Dynamic Simulator Scenarios; no dates  
RP-BY-1000; Maintenance Care and Inspection of the ISI Viking Self-Contained Breathing
Apparatus (SCBA), Revision 9
Self-Contained Breathing Apparatus Monthly Inspection, September 2008
Byron Station Fire Drill Critique Form, August 24, 2008
Summary Report for Each Shift Reflecting Fire Brigade and HazMat Qualification Status,
October 12, 2008
IR 823253; Safe-Guards Information Slows Fire Response, September 27, 2008
Section 1R07: Heat Sink Performance
WO 1036955; Perform As-Found/As-Left Inspections of 2C RCFC
Issue 830146; Replace RCFC Channel Heads with stainless Steel in B2R15, October 13, 2008
IR 830370; Restricted Tubes in 2C RCFC, Need to Plug, October 13, 2008
IR 829315; 2C RCFC Channel Head Degradation, Divider Plates, October 10, 2008
Section 1R08: Inservice Inspection Activities
IR 829647; Penetration 41 Not Examined During B2R13; October 11, 2008
IR 831084; Foreign Objects Found In 2C SG Secondary Side - B2R14; October 15, 2008
IR 829610; Acceptance Criteria Used On SX Pipe Was Not Appropriate; October 11, 2008
IR 843635, Steam Generator Tube Sheet Inspection Results - B2R14, November 11, 2008
IR 832181; Foreign Objects Found In 2A SG Secondary - B2R14; dated October 17, 2008
IR 830452; B2R14 - Weld Defects Revealed During Radiography Of Repair; October 14, 2008
IT00717275-02; Buildup of Deposits in Steam Generators, NRC IN 2007-37
ER-AP-335-1012; Bare Metal Visual Examination of PWR Vessel Penetration and Nozzle Safe-
Ends; Revision 3
ER-AP-335-040; Evaluation of Eddy Current Data for Steam Generator Tubing; Revision 4
EXE-ISI-11; Liquid Penetrant Examination, Revision 4
EXE-UT-350; Procedure for Acquiring Material Thickness and Weld Contours; Revision 2
EXE-PDI-UT-2; Ultrasonic Examination of Austenitic Piping Welds in Accordance with PDI-UT-
2; Revision 5
EXAE-ISI-8; VT-1 Direct; Revision 1
ER-AP-335-039; Multi-Frequency Eddy Current Data Acquisition of Steam Generator Tubing;
Revision 5
ER-MW-335-1009; Site Specific Performance; Revision 4
ER-AP-331; Boric Acid Corrosion Control (BACC) Program; Revision 3
ER-AP-331-1001; Boric Acid Corrosion control (BACC) Inspection Locations, Implementation
and Inspection Guidelines; Revision 3
ER-AP-331-1002; Boric Acid Corrosion control Program Identification, Screening, and
Evaluation; Revision 4
ER-AP-331-1004; Boric Acid Corrosion Control (BACC) Training and Qualification, Revision 2
ER-AP-420-002; Byron/Braidwood Unit 2: Steam Generator Eddy Current Activities; Revision 8
Section 1R11: Licensed Operator Requalification Program
Six Reactor Operator Biennial Written Examinations for CY 2008; no dates
Thirty Senior Reactor Operator Examination Questions for CY 2008 Exams; no dates
Twelve Dynamic Simulator Scenarios; no dates
                                                3                                Attachment


 
48 Job Performance Measures; no dates
Attachment
Licensed Operator Written Examination and Operating Test Results, CY 2008; no date
448 Job Performance Measures; no dates Licensed Operator Written Examination and Operating Test Results, CY 2008; no date  
Section 1R12: Maintenance Effectiveness
Section 1R12: Maintenance Effectiveness
IR 417274; Hydramotor Indication Shows Open but Damper Blades are Closed, March 11, 2002 IR 460411; VA Supply/Exhaust Fan Vibration Alarm Setpoint Basis Concern  
IR 417274; Hydramotor Indication Shows Open but Damper Blades are Closed, March 11, 2002
IR 717005; VA-Tolerance for Equipment Degradation, January 1, 2008  
IR 460411; VA Supply/Exhaust Fan Vibration Alarm Setpoint Basis Concern
 
IR 717005; VA-Tolerance for Equipment Degradation, January 1, 2008
IR 726481; High Vibrations on 0C VA Fan (Supply Fan), January 24, 2008  
IR 726481; High Vibrations on 0C VA Fan (Supply Fan), January 24, 2008
 
IR 727128; VA Issues, January 26, 2008
IR 727128; VA Issues, January 26, 2008  
IR 735812; VA Concerns, February 13, 2001
 
IR 748406; Need (A)(1) Determination: VA Unacceptable Performance Trend, March 12, 2008
IR 735812; VA Concerns, February 13, 2001 IR 748406; Need (A)(1) Determination: VA Unacceptable Performance Trend, March 12, 2008 IR 850742; Control Damper Problems for 1A DG Ventilation, December 01, 2008  
IR 850742; Control Damper Problems for 1A DG Ventilation, December 01, 2008
IR 869580; MM Expanded Scope Replace Linear Converter, January 23, 2007  
IR 869580; MM Expanded Scope Replace Linear Converter, January 23, 2007
IR 999934; Replace Linear Converter, November 07, 2008  
IR 999934; Replace Linear Converter, November 07, 2008
WO 99270872; 1A DG Vent Outside Damp Not Fully Closed, September 13, 2008 VA Degradation/Status Presentations to the Plant Health Committee, December 10, 2007, February 4, 2008, and May 5, 2008  
WO 99270872; 1A DG Vent Outside Damp Not Fully Closed, September 13, 2008
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
VA Degradation/Status Presentations to the Plant Health Committee, December 10, 2007,
 
February 4, 2008, and May 5, 2008
Unit 1 Risk Configurations; Week of October 13, 2008, Revision 3 Unit 2 Risk Configurations; Week of November 17, 2008  
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Protected Equipment Log for 2B DG Outage, October 11, 2008  
Unit 1 Risk Configurations; Week of October 13, 2008, Revision 3
Protected Equipment Log for Line 0622/Bus 12 Outage, October 12, 2008  
Unit 2 Risk Configurations; Week of November 17, 2008
Protected Equipment Log for Unit 0 Component Cooling Water Heat Exchanger,  
Protected Equipment Log for 2B DG Outage, October 11, 2008
October 11, 2008 Protected Equipment Log for Unit 2 CC Heat Exchanger, November 16, 2008 Protected Equipment Log for 2RA RH Pump Suction OOS, November 17, 2008  
Protected Equipment Log for Line 0622/Bus 12 Outage, October 12, 2008
B2R14 Shutdown Risk Evaluation; October 15, 2008  
Protected Equipment Log for Unit 0 Component Cooling Water Heat Exchanger,
B2R14 Outage Status, October 16, 2008  
October 11, 2008
Byron Operations Log; October 15, 2008, to October 16, 2008 OU-AP-104; Shutdown Safety Management Program Byron/Braidwood Annex, Revision 11 IR 832167; NOS Identified OPS Lacks Sensitivity to OLR/SDR, October 17, 2008  
Protected Equipment Log for Unit 2 CC Heat Exchanger, November 16, 2008
Unit 0/1/2 Standing Order; Operator Ownership During IMD Surveillances, October 17, 2008  
Protected Equipment Log for 2RA RH Pump Suction OOS, November 17, 2008
IR 829481; NOS ID Shutdown Risk Vulnerability, October 10, 2008  
B2R14 Shutdown Risk Evaluation; October 15, 2008
B2R14 Outage Status, October 16, 2008
Byron Operations Log; October 15, 2008, to October 16, 2008
OU-AP-104; Shutdown Safety Management Program Byron/Braidwood Annex, Revision 11
IR 832167; NOS Identified OPS Lacks Sensitivity to OLR/SDR, October 17, 2008
Unit 0/1/2 Standing Order; Operator Ownership During IMD Surveillances, October 17, 2008
IR 829481; NOS ID Shutdown Risk Vulnerability, October 10, 2008
Section 1R15: Operability Evaluations
IR 810117; Unit 1 LM Indicates Potential Source of Noise as Near 1RC8002D, August 22, 2008
IR 810867; Expansion Tank Overflow When Started and Running, August 26, 2008
IR 814019; Low JW Level in the 1B AF Pump, September 04, 2008
IR 846398; Need Work Order Created to Replace Grease, November 18, 2008
IR 846420; 2SI8811A; Motor Found Degraded Per Inspection Criteria, November 18, 2008
EC 366163; Operations Evaluation 07-005, Unventable Gas Voids in Containment Recirculation
Sump Piping, November 20, 2008
EC 371879; Operations Evaluation 08-007, Gas Void at 2CS009A, November 20, 2008
EC 371965; Operations Evaluation 08-008, 2B AF Pump Jacket Water Overflow, Revision 000
EC 373393; Operations Evaluation 08-010, 1B DG Cylinder and Head Indications,
December 18, 2008
Fluid Analysis Report; Unit 2 AF Cooler, September 24, 2008
                                              4                                Attachment


Section 1R15: Operability Evaluations
Operational and Technical Decision Making 2008 - 2009; Suspect 1RC8002D Valve guide(s)
IR 810117; Unit 1 LM Indicates Potential Source of Noise as Near 1RC8002D, August 22, 2008
Not Properly Retained in Valve Body
IR 810867; Expansion Tank Overflow When Started and Running, August 26, 2008
Adverse Condition Monitoring and Contingency Plan; Unit 1 Loose Parts Monitoring System
IR 814019; Low JW Level in the 1B AF Pump, September 04, 2008
(LPMS) Noise, August 26, 2008
IR 846398; Need Work Order Created to Replace Grease, November 18, 2008
CAE-02-31 Westinghouse Letter; LSIV Loose Parts 50.59 Screen EVAL-02-062, Revision 1,
IR 846420; 2SI8811A; Motor Found Degraded Per Inspection Criteria, November 18, 2008 EC 366163; Operations Evaluation 07-005, Unventable Gas Voids in Containment Recirculation Sump Piping, November 20, 2008
March 21, 2002
EC 371879; Operations Evaluation 08-007, Gas Void at 2CS009A, November 20, 2008
WO 1072112 02; MOV PM, Actuator Inspection, Diagnostic testing, November 18, 2008
EC 371965; Operations Evaluation 08-008, 2B AF Pump Jacket Water Overflow, Revision 000
Section 1R18: Plant Modifications
 
IR 842362; 2CV181 2A RCP Standpipe PW Supply Valve Failed to Close, November 08, 2008
EC 373393; Operations Evaluation 08-010, 1B DG Cylinder and Head Indications, December 18, 2008
IR 843783; Unexpected Alarm, November 12, 2008
Fluid Analysis Report; Unit 2 AF Cooler, September 24, 2008 
IR 846404; Revised Bars for TCP 373002 are Incorrect, November 18, 2008
Attachment
EC 373002; Installation of Temporary Line to Connect the Drain Lines of RCP Standpipes 2A
5Operational and Technical Decision Making 2008 - 2009; Suspect 1RC8002D Valve guide(s) Not Properly Retained in Valve Body  
and 2D, Revision 0
Adverse Condition Monitoring and Contingency Plan; Unit 1 Loose Parts Monitoring System (LPMS) Noise, August 26, 2008 CAE-02-31 Westinghouse Letter; LSIV Loose Parts 50.59 Screen EVAL-02-062, Revision 1,  
EC 371360; Install Vent Valve on 2SI05CA-8, Revision 2
March 21, 2002  
EC 373224; Provide Temporary Fans for 1A DG Room, Revision 0
WO 1072112 02; MOV PM, Actuator Inspection, Diagnostic testing, November 18, 2008  
WO 01149077; Install Vent Valve on 2SI05CA-8, October 18, 2008
 
WO 01149077 13; SEP PMT: VT-2 of 2SI130, October 15, 2008
Section 1R18: Plant Modifications
WO 01149077 14; OP PMT: Verify No Seat leakage on 2SI130, October 15, 2008
IR 842362; 2CV181 "2A RCP Standpipe PW Supply Valve" Failed to Close, November 08, 2008 IR 843783; Unexpected Alarm, November 12, 2008  
WO 01149077 15; SEP PMT: Record Vibe Data 2SI130 at Full Flow Conditions,
IR 846404; Revised Bars for TCP 373002 are Incorrect, November 18, 2008  
October 15, 2008
EC 373002; Installation of Temporary Line to Connect the Drain Lines of RCP Standpipes 2A  
Section 1R19: Post Maintenance Testing
 
1BOSR 3.2.8-610B; Unit 1 ESFAS Instrumentation Slave Relay Surveillance and Automatic
and 2D, Revision 0 EC 371360; Install Vent Valve on 2SI05CA-8, Revision 2 EC 373224; Provide Temporary Fans for 1A DG Room, Revision 0  
Actuation Test (Train B Automatic Safety Injection - K610), Revision 2
WO 01149077; Install Vent Valve on 2SI05CA-8, October 18, 2008  
2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Emergency Actuation Signal
WO 01149077 13; SEP PMT: VT-2 of 2SI130, October 15, 2008  
Verification Test, Revision 4
WO 01149077 14; OP PMT: Verify No Seat leakage on 2SI130, October 15, 2008 WO 01149077 15; SEP PMT: Record Vibe Data 2SI130 at Full Flow Conditions, October 15, 2008  
Section 1R19: Post Maintenance Testing
  1BOSR 3.2.8-610B; Unit 1 ESFAS Instrumentation Slave Relay Surveillance and Automatic Actuation Test (Train B Automatic Safety Injection - K610), Revision 2  
2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Emergency Actuation Signal Verification Test, Revision 4  
WO 999110; 1AP12E-A Relay #1-RCF2 for 1VP01CB Operations PMT Partial 1BOSR 3.2.8-
WO 999110; 1AP12E-A Relay #1-RCF2 for 1VP01CB Operations PMT Partial 1BOSR 3.2.8-
610B, November 25, 2008 2BOSR 3.2.8-632A; ESFAS Instrumentation Slave Relay Surveillance (Train A Auxiliary Feedwater Actuation - Relays k632, K639, Revision 2  
610B, November 25, 2008
2BOSR 3.2.8-632A; ESFAS Instrumentation Slave Relay Surveillance (Train A Auxiliary
Feedwater Actuation - Relays k632, K639, Revision 2
WO 1165207 01; MM-Repair of 2SI8818C During B2R14
WO 1165207 04; EP - Perform Visual Examination of Disassembled Check Valve
WO 1165207 06; Operations PMT - 2SI8818C SLT Per 2BOSR 4.14.1-1
WO 1165207 07; Operations PMT - 2SI8818C CO Per 2BOSR 5.5.8RH.2-2
WO 1020023 01; 2RH25 VT-2 Exam, October 15, 2008
ASME Section XI Repair/Replacement Plan; 2SI8818C (Loop 3 Cold Leg Accumulation
Injection Check Valve, September 29, 2008
BOP CV-19; Switching Charging Pumps, Revision 14
1BOSR 5.5.1-1; Unit 1 RCS Seal Injection Flow Verification Monthly Surveillance, Revision 4
2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4
Section 1R20: Refueling and Outage Activities
Ultrasonic Thickness Calibration Data Sheet; Report Number 2008-707
IR 826879; Calibrate/Repair 2FI-0928A, October 05, 2008
IR 834405; Need B2R15 W/O to Retrieve Rag and Wire From Upender Pit
B2R14 Work Orders Added to Date, October 15, 2008
                                                5                                  Attachment


WO 1165207 01; MM-Repair of 2SI8818C During B2R14
List of Work Orders Removed from B2R14 via SCARF Process as of 7:00 am on
WO 1165207 04; EP - Perform Visual Examination of Disassembled Check Valve
October 16, 2008
 
1BGP 100-2; Plant Startup, Revision 37
WO 1165207 06; Operations PMT - 2SI8818C SLT Per 2BOSR 4.14.1-1
1BGP 100-2A1; Reactor Startup, Revision 26
WO 1165207 07; Operations PMT - 2SI8818C CO Per 2BOSR 5.5.8RH.2-2 WO 1020023 01; 2RH25 VT-2 Exam, October 15, 2008 ASME Section XI Repair/Replacement Plan; 2SI8818C (Loop 3 Cold Leg Accumulation
1BGP 100-2TI; Plant Startup Flowchart, Revision 10
Injection Check Valve, September 29, 2008
1BGP 100-2T3; Reactor Startup Flowchart, Revision 5
BOP CV-19; Switching Charging Pumps, Revision 14
1BGP 100-4; Power Descension, Revision 36
1BOSR 5.5.1-1; Unit 1 RCS Seal Injection Flow Verification Monthly Surveillance, Revision 4 2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4
1BGP 100-4T1; Power Descension Flowchart, Revision 11
Section 1R20: Refueling and Outage Activities
1BGP 100-5; Plant Shutdown and Cooldown, Revision 53
Ultrasonic Thickness Calibration Data Sheet; Report Number 2008-707 IR 826879; Calibrate/Repair 2FI-0928A, October 05, 2008
1BGP 100-5TI; Plant Shutdown and Cooldown Flowchart, Revision 26
IR 834405; Need B2R15 W/O to Retrieve Rag and Wire From Upender Pit
BOP RH-6; Operation of the RH System in Shutdown Cooling, Revision 36
B2R14 Work Orders Added to Date, October 15, 2008 
BOP RH-8; Filling the Refueling Cavity for Refueling, Revision 18
Attachment
BOP RH-9; Pump Down of the Refueling Cavity to the RWST, Revision 24
6List of Work Orders Removed from B2R14 via SCARF Process as of 7:00 am on  
ALM Corporation Material Handling Platform Lift Manual
October 16, 2008  
BAP 1450-1; Access to Containment, Revision 37
1BGP 100-2; Plant Startup, Revision 37 1BGP 100-2A1; Reactor Startup, Revision 26 1BGP 100-2TI; Plant Startup Flowchart, Revision 10  
2BOSR Z.5.B.1-1; Containment Loose Debris Inspection, Revision 0
1BGP 100-2T3; Reactor Startup Flowchart, Revision 5  
Issue 834555; B2R14 Reactor Cavity Hoist Cable Ties, October 22, 2008
1BGP 100-4; Power Descension, Revision 36  
LS-AA-125; Corrective Action Program Procedure, Revision 12
1BGP 100-4T1; Power Descension Flowchart, Revision 11  
IR 833539; White Plastic Cable Tie Not Immediately Retrievable, October 20, 2008
1BGP 100-5; Plant Shutdown and Cooldown, Revision 53 1BGP 100-5TI; Plant Shutdown and Cooldown Flowchart, Revision 26 BOP RH-6; Operation of the RH System in Shutdown Cooling, Revision 36  
IR 834002; Foreign Material in 2B ECCS Recirculation Sump, October 21,2008
BOP RH-8; Filling the Refueling Cavity for Refueling, Revision 18  
IR 834087; Loose Debris Walkdown Items Requiring Disposition, October 21, 2008
BOP RH-9; Pump Down of the Refueling Cavity to the RWST, Revision 24  
IR 835427; B2R14 LL - Weakness in Control of Material Left in Containment, October 23, 2008
ALM Corporation Material Handling Platform Lift Manual BAP 1450-1; Access to Containment, Revision 37 2BOSR Z.5.B.1-1; Containment Loose Debris Inspection, Revision 0  
EC 372856; Evaluation of Foreign Material in Unit 2 Containment Building, November 12, 2008
Issue 834555; B2R14 Reactor Cavity Hoist Cable Ties, October 22, 2008  
Corrective Action Documents as a Result of NRC Inspection
LS-AA-125; Corrective Action Program Procedure, Revision 12  
IR 833612; Inactive Boric Acid Leak on 2SI8822C, October 20, 2008
IR 833539; White Plastic Cable Tie Not Immediately Retrievable, October 20, 2008 IR 834002; Foreign Material in 2B ECCS Recirculation Sump, October 21,2008 IR 834087; Loose Debris Walkdown Items Requiring Disposition, October 21, 2008  
IR 833613; Inactive Boric Acid Leak on 2SI8810C, October 20, 2008
IR 835427; B2R14 LL - Weakness in Control of Material Left in Containment, October 23, 2008  
IR 833881; Inactive Boric Acid Leak, System Not Verified At This Time, October 21, 2008
EC 372856; Evaluation of Foreign Material in Unit 2 Containment Building, November 12, 2008  
IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008
IR 856813; Operator Missing a Cover During Mode 4 Walkdown, December 16, 2008
IR 856819; 2LL091E Trickle Charge Light Is Out, December 16, 2008
IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008
Section 1R22: Surveillance Testing
1BOSR 6.1.1-11; Primary Containment Type C Local Leakage Rate Tests and IST Tests of
Pressurizer Relief System Partial for 1RY8028, Revision 7
2BOSR 7.5.4-2; Unit 2 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance,
Revision 16
2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Verification Test, Revision 4
2BOSR 8.1.2-1; Unit 2 A Diesel Generator Operability Surveillance, Revision 21
2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4
WO 1024422 01; 2B Diesel Generator SI Signal Override Test, October 14, 2008
WO 1028733 01; Reactor Coolant System CheckValve Leakage Surveillance, October 21, 2008
WO 1157684 01; 1CV01PB Group A IST Requirement for CV Pump, November 06, 2008
Byron Inservice Testing Bases Document; Valve EPN 2SI8818A-D, Loop A-D Cold Leg
Accumulator Injection Check Valve
Byron Inservice Testing Bases Document; Valve EPN 2SI8948A, Accumulator Outlet to RC
Loop Second Check Valve
                                              6                                    Attachment


BOP DG-11; Diesel Generator Startup, Revision 20
BOP DG-12; Diesel Generator Shutdown, Revision 19
Corrective Action Documents as a Result of NRC Inspection
Corrective Action Documents as a Result of NRC Inspection
IR 833612; Inactive Boric Acid Leak on 2SI8822C, October 20, 2008 IR 833613; Inactive Boric Acid Leak on 2SI8810C, October 20, 2008
IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 06, 2008
IR 833881; Inactive Boric Acid Leak, System Not Verified At This Time, October 21, 2008
IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 07, 2008
IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008
Section 2OS1: Access Control to Radiologically Significant Areas
IR 856813; Operator Missing a Cover During Mode 4 Walkdown, December 16, 2008 IR 856819; 2LL091E Trickle Charge Light Is Out, December 16, 2008 IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008
RP-AA-460; Controls for High Radiation and Locked High Radiation Areas; Revision 17
 
RP-AA-460-001; Controls for Very High Radiation Areas; Revision 1
Section 1R22: Surveillance Testing
RP-AA-460; Access to Reactor Incore Sump Area; Revision 2
1BOSR 6.1.1-11; Primary Containment Type C Local Leakage Rate Tests and IST Tests of Pressurizer Relief System "Partial for 1RY8028", Revision 7
RP- BY-500-1003; Radiological Controls for Handling Items and Hanging Activated Parts in the
2BOSR 7.5.4-2; Unit 2 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance, Revision 16
Spent Fuel Pool
2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Verification Test, Revision 4
Radiation Work Permit and Associated ALARA Reviews; RWP 10008926; B2R14 Seal Table -
2BOSR 8.1.2-1; Unit 2 A Diesel Generator Operability Surveillance, Revision 21
Rack Disconnect/Maintenance/Eddy Current/Restoration
2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4 WO 1024422 01; 2B Diesel Generator SI Signal Override Test, October 14, 2008 WO 1028733 01; Reactor Coolant System CheckV
Radiation Work Permit and Associated ALARA Reviews; RWP 10009830; P-68 Penetrant Test
alve Leakage Surveillance, October 21, 2008 WO 1157684 01; 1CV01PB Group A IST Requirement for CV Pump, November 06, 2008
and Vent Line Inspection
Byron Inservice Testing Bases Document; Valve EPN 2SI8818A-D, Loop A-D Cold Leg
IR 795311; RWP Violations (PC Requirements); dated July 10, 2008
Accumulator Injection Check Valve
IR 761294; Level 1 Personal Contamination Event; dated 9, 2008
Byron Inservice Testing Bases Document; Valve EPN 2SI8948A, Accumulator Outlet to RC
IR 756342; Worker Entered A/D Platform without Electronic Dosimeter; dated March 29, 2008
Loop Second Check Valve
IR 754696; Worker Locked Out of RCA - Rad Worker Behavior; dated March 26, 2008
 
IR 756136; PCE: B1R15 Personal Contamination Event; dated March 28, 2008
Attachment
IR 673712; RP Not Effectively Using Corrective Action Program; dated September 20, 2007
7BOP DG-11; Diesel Generator Startup, Revision 20 BOP DG-12; Diesel Generator Shutdown, Revision 19
IR 755986; Alpha Survey Documentation Gaps; dated March 27, 2008
 
IR 756296; RP-AA-460-1001; Not Completed in Timely Manner; dated March 28, 2008
Corrective Action Documents as a Result of NRC Inspection
IR 812338; Ni-63 Source Leak Tests Exceed 6-Month Surveillance Frequency; dated
IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 06, 2008 IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 07, 2008  
August 22, 2008
 
Section 1EP6: Drill Evaluation
Section 2OS1: Access Control to Radiologically Significant Areas
IR 844467; OSC Minimum Staffing Not Met for Crew D in Drill, November 13, 2008
RP-AA-460; Controls for High Radiation and Locked High Radiation Areas; Revision 17 RP-AA-460-001; Controls for Very High Radiation Areas; Revision 1 RP-AA-460; Access to Reactor Incore Sump Area; Revision 2  
Byron 2008 Drive-In Drill; Scenario Information
RP- BY-500-1003; Radiological Controls for Handling Items and Hanging Activated Parts in the  
Nuclear Accident Reporting System (NARS) Form; Utility Message No. 2, November 12, 2008
 
Issue 844467; OSC Minimum Staffing Not Met for During Drill, November 12, 2008
Spent Fuel Pool  
Section 4OA1: Performance Indicator Verification
Radiation Work Permit and Associated ALARA Reviews; RWP 10008926; B2R14 Seal Table - Rack Disconnect/Maintenance/Eddy Current/Restoration Radiation Work Permit and Associated ALARA Reviews; RWP 10009830; P-68 Penetrant Test  
LS-AA-2090; Monthly Data Elements for NRC Reactor Coolant System (RCS) Specific Activity;
and Vent Line Inspection  
dated July 3, 2007 through September 2, 2008
IR 795311; RWP Violations (PC Requirements); dated July 10, 2008  
LS-AA-2100; Monthly Data Elements for NRC Reactor Coolant System Leakage, Revision 5
IR 761294; Level 1 Personal Contamination Event; dated 9, 2008 IR 756342; Worker Entered A/D Platform without Electronic Dosimeter; dated March 29, 2008 IR 754696; Worker Locked Out of RCA - Rad Worker Behavior; dated March 26, 2008  
LS-AA-2150; Monthly Data Elements for RETS/ODCM Radiological Effluent Occurrences; dated
IR 756136; PCE: B1R15 Personal Contamination Event; dated March 28, 2008  
July 10, 2007 through September 10, 2008
IR 673712; RP Not Effectively Using Corrective Action Program; dated September 20, 2007  
MSPI Derivation Report; Unit 1 and Unit 2 High Pressure Injection System Unavailability and
IR 755986; Alpha Survey Documentation Gaps; dated March 27, 2008  
Unreliability Index, February 2008
IR 756296; RP-AA-460-1001; Not Completed in Timely Manner; dated March 28, 2008 IR 812338; Ni-63 Source Leak Tests Exceed 6-Month Surveillance Frequency; dated August 22, 2008  
Operations Log; February 01, 2008 - February 29, 2008
Section 1EP6: Drill Evaluation
MSPI Derivation Report; Unit 1 and Unit 2 Cooling Water System Unavailability and Unreliability
IR 844467; OSC Minimum Staffing Not Met for Crew D in Drill, November 13, 2008 Byron 2008 Drive-In Drill; Scenario Information Nuclear Accident Reporting System (NARS) Form; Utility Message No. 2, November 12, 2008  
Index, March 2008
Issue 844467; OSC Minimum Staffing Not Met for During Drill, November 12, 2008  
IR 854124; Inconsequential Error identified in March 2008 MSPI Data for SX,
Section 4OA1: Performance Indicator Verification
December 09, 2008
LS-AA-2090; Monthly Data Elements for NRC Reactor Coolant System (RCS) Specific Activity; dated July 3, 2007 through September 2, 2008 LS-AA-2100; Monthly Data Elements for NRC Reactor Coolant System Leakage, Revision 5 LS-AA-2150; Monthly Data Elements for RETS/ODCM Radiological Effluent Occurrences; dated  
                                                7                                Attachment
 
July 10, 2007 through September 10, 2008  
MSPI Derivation Report; Unit 1 and Unit 2 High Pressure Injection System Unavailability and Unreliability Index, February 2008  
Operations Log; February 01, 2008 - February 29, 2008  
MSPI Derivation Report; Unit 1 and Unit 2 Cooling Water System Unavailability and Unreliability  
Index, March 2008  
IR 854124; Inconsequential Error identified in March 2008 MSPI Data for SX,  
December 09, 2008
Attachment  
8Operations Log; March 01, 2008 - March 31, 2008 MSPI Derivation Report; Unit 1 and Unit 2 Residual Heat Removal System Unavailability and
Unreliability Index, July 2008
Operations Log; July 01, 2008 - July 31, 2008 MSPI Derivation Report; Unit 1 and Heat Removal System Unavailability and Unreliability Index,
October 2007
Operations Log; October 01, 2007 - October 31, 2007
MSPI Derivation Report; Unit 1 and Unit 2 Heat Removal System Unavailability and Unreliability
 
Index, April 2008 Operations Log; March 01, 2008 - March 31, 2008 Operations Log; October 01, 2007 - October 31, 2007
MSPI Derivation Report; Unit 1 and Unit 2 Emergency AC Power System Unavailability and
Unreliability Index, June 2008
Operations Log, June 01, 2008 - June 30, 2008
Section 4OA2: Identification and Resolution of Problems
IR 642107; IST Program Implementation, June 19, 2007 IR 678543; Possible Pre-Conditioning Issue - IST Testing, October 1, 2007
IR 686518; Byron Review of Braidwood Potential Pre-Conditioning Issue, October 18, 2007 ER-AA-302-1006; Generic Letter 96-05 Program Motor-Operated Valve Maintenance and
Testing Guidelines, Revision 7


Section 4OA5: Other Activities
Operations Log; March 01, 2008 - March 31, 2008
1BOSR 8.1.14-1; Unit 1A Diesel Generator 24 Hour Endurance Run, Revision 10  
MSPI Derivation Report; Unit 1 and Unit 2 Residual Heat Removal System Unavailability and
1BOSR 8.1.14-2; Unit 1B Diesel Generator 24 Hour Endurance Run, Revision 8  
Unreliability Index, July 2008
2BOSR 8.1.14-1; Unit 2A Diesel Generator 24 Hour Endurance Run, Revision 10  
Operations Log; July 01, 2008 - July 31, 2008
2BOSR 8.1.14-2; Unit 2B Diesel Generator 24 Hour Endurance Run, Revision 10  
MSPI Derivation Report; Unit 1 and Heat Removal System Unavailability and Unreliability Index,
Calculation 19-T-5; Diesel Generator Loading During LOOP/LOCA, Revision 6  
October 2007
Operations Log; October 01, 2007 - October 31, 2007
MSPI Derivation Report; Unit 1 and Unit 2 Heat Removal System Unavailability and Unreliability
Index, April 2008
Operations Log; March 01, 2008 - March 31, 2008
Operations Log; October 01, 2007 - October 31, 2007
MSPI Derivation Report; Unit 1 and Unit 2 Emergency AC Power System Unavailability and
Unreliability Index, June 2008
Operations Log, June 01, 2008 - June 30, 2008
Section 4OA2: Identification and Resolution of Problems
IR 642107; IST Program Implementation, June 19, 2007
IR 678543; Possible Pre-Conditioning Issue - IST Testing, October 1, 2007
IR 686518; Byron Review of Braidwood Potential Pre-Conditioning Issue, October 18, 2007
ER-AA-302-1006; Generic Letter 96-05 Program Motor-Operated Valve Maintenance and
Testing Guidelines, Revision 7
Section 4OA5: Other Activities
1BOSR 8.1.14-1; Unit 1A Diesel Generator 24 Hour Endurance Run, Revision 10
1BOSR 8.1.14-2; Unit 1B Diesel Generator 24 Hour Endurance Run, Revision 8
2BOSR 8.1.14-1; Unit 2A Diesel Generator 24 Hour Endurance Run, Revision 10
2BOSR 8.1.14-2; Unit 2B Diesel Generator 24 Hour Endurance Run, Revision 10
Calculation 19-T-5; Diesel Generator Loading During LOOP/LOCA, Revision 6
                                              8                                  Attachment


 
                        LIST OF ACRONYMS USED
Attachment
AFW   Auxiliary Feedwater System
9 LIST OF ACRONYMS USED  
ALARA As Low As Reasonably Achievable
CAP   Corrective Action Program
AFW Auxiliary Feedwater System ALARA As Low As Reasonably Achievable  
CFR   Code of Federal Regulations
CAP Corrective Action Program  
JPM   Job Performance Measure
CFR Code of Federal Regulations  
IMC   Inspection Manual Chapter
JPM Job Performance Measure
IP   Inspection Procedure
IMC Inspection Manual Chapter IP Inspection Procedure IR Inspection Report  
IR   Inspection Report
IR Issue Report  
IR   Issue Report
IST Inservice Testing  
IST   Inservice Testing
LORT Licensed Operator Requalification Training MSPI Mitigating Systems Performance Index NCV Non-Cited Violation  
LORT Licensed Operator Requalification Training
NEI Nuclear Energy Institute  
MSPI Mitigating Systems Performance Index
NRC U.S. Nuclear Regulatory Commission  
NCV   Non-Cited Violation
OOS Out of Service ODCM Offsite Dose Calculation Manual OSP Outage Safety Plan  
NEI   Nuclear Energy Institute
PI Performance Indicator  
NRC   U.S. Nuclear Regulatory Commission
RCFC Reactor Containment Fan Cooler  
OOS   Out of Service
RCS Reactor Coolant System  
ODCM Offsite Dose Calculation Manual
RETS Radiological Effluent Technical Specifications RWP Radiation Work Permit SDP Significance Determination Process  
OSP   Outage Safety Plan
TI Temporary Instructions  
PI   Performance Indicator
TS Technical Specification  
RCFC Reactor Containment Fan Cooler
UFSAR Updated Final Safety Analysis Report URI Unresolved Item WO Work Order
RCS   Reactor Coolant System
RETS Radiological Effluent Technical Specifications
RWP   Radiation Work Permit
SDP   Significance Determination Process
TI   Temporary Instructions
TS   Technical Specification
UFSAR Updated Final Safety Analysis Report
URI   Unresolved Item
WO   Work Order
                                      9            Attachment
}}
}}

Revision as of 09:00, 14 November 2019

IR 05000454-08-005, 05000455-08-005; Exelon Generation Company, LLC; October 1 - December 31, 2008; Byron Station, Units 1 & 2; Refueling and Other Outage Activities, and Access Control to Radiologically Significant Areas
ML090420213
Person / Time
Site: Byron  Constellation icon.png
Issue date: 02/10/2009
From: Richard Skokowski
Region 3 Branch 3
To: Pardee C
Exelon Generation Co, Exelon Nuclear
References
IR-08-005
Download: ML090420213 (49)


See also: IR 05000454/2008005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

February 10, 2009

Mr. Charles G. Pardee

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville IL 60555

SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION

REPORT 05000454/2008-005 05000455/2008-005

Dear Mr. Pardee:

On December 31, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an

integrated inspection at your Byron Station, Units 1 and 2. The enclosed inspection report

documents the inspection findings which were discussed on January 15, 2009, with

Mr. D. Hoots and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, two NRC-identified findings of very low safety

significance were identified. The findings involved violations of NRC requirements. However,

because of their very low safety significance, and because the issues were entered into your

corrective action program, the NRC is treating the issues as Non-Cited Violations in accordance

with Section VI.A.1 of the NRC Enforcement Policy. Furthermore, four licensee identified

violations are listed in Section 4OA7 of this report.

If you contest the subject or severity of a Non-Cited Violation, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial,

to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the Resident Inspector Office at the Byron Station.

C. Pardee -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS)

component of NRC's document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Richard A. Skokowski, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-454; 50-455

License Nos. NPF-37; NPF-66

Enclosure: Inspection Report No. 05000454/2008-005 and 05000455/2008-005

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Byron Station

Plant Manager - Byron Station

Manager Regulatory Assurance - Byron Station

Senior Vice President - Midwest Operations

Senior Vice President - Operations Support

Vice President - Licensing and Regulatory Affairs

Director - Licensing and Regulatory Affairs

Manager Licensing - Braidwood, Byron, and LaSalle

Associate General Counsel

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

J. Klinger, State Liaison Officer,

Illinois Emergency Management Agency

P. Schmidt, State Liaison Officer, State of Wisconsin

Chairman, Illinois Commerce Commission

B. Quigley, Byron Station

C. Pardee -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter,

its enclosure and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS)

component of NRC's document system (ADAMS), accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

Richard A. Skokowski, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-454; 50-455

License Nos. NPF-37; NPF-66

Enclosure: Inspection Report No. 05000454/2008-005 and 05000455/2008-005

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Byron Station

Plant Manager - Byron Station

Manager Regulatory Assurance - Byron Station

Senior Vice President - Midwest Operations

Senior Vice President - Operations Support

Vice President - Licensing and Regulatory Affairs

Director - Licensing and Regulatory Affairs

Manager Licensing - Braidwood, Byron, and LaSalle

Associate General Counsel

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

J. Klinger, State Liaison Officer,

Illinois Emergency Management Agency

P. Schmidt, State Liaison Officer, State of Wisconsin

Chairman, Illinois Commerce Commission

B. Quigley, Byron Station

DOCUMENT NAME: G:\1-SECY\1-WORK IN PROGRESS\BYRO 2008 005.DOC

G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII

NAME RSkokowski:dtp

DATE 02/10/09

OFFICIAL RECORD COPY

Letter to C. Pardee from R. Skokowski dated February 10, 2009

SUBJECT: BYRON STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT

05000454/2008-005 05000455/2008-005

DISTRIBUTION:

Tamara Bloomer

RidsNrrDorlLpl3-2

RidsNrrPMByron Resource

RidsNrrDirsIrib Resource

Mark Satorius

Kenneth OBrien

Jared Heck

Allan Barker

Carole Ariano

Linda Linn

Cynthia Pederson

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports@nrc.gov

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-454; 50-455

License Nos: NPF-37; NPF-66

Report Nos: 05000454/2008-005 and 05000455/2008-005

Licensee: Exelon Generation Company, LLC

Facility: Byron Station, Units 1 and 2

Location: Byron, IL

Dates: October 1, 2008, through December 31, 2008

Inspectors: B. Bartlett, Senior Resident Inspector

R. Ng, Resident Inspector

J. Cassidy, Senior Health Physicist

A. Dunlop, Reactor Inspector

B. Jones, Reactor Inspector

D. Jones, Reactor Inspector

R. Langstaff, Reactor Inspector

D. McNeil, Reactor Inspector

R. Winter, Reactor Inspector

C. Thompson, Resident Inspector

Illinois Department of Emergency Management

Observer: J. Gilliam, Reactor Engineer

Approved by: R. Skokowski, Chief

Branch 3

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS 1

REPORT DETAILS .3

Summary of Plant Status .3

1. REACTOR SAFETY .....3

1R01 Adverse Weather Protection (71111.01) .....................................................3

1R04 Equipment Alignment (71111.04) ................................................................4

1R05 Fire Protection (71111.05)...........................................................................4

1R06 Flooding (71111.06) .....6

1R07 Annual Heat Sink Performance (71111.07).................................................6

1R11 Licensed Operator Requalification Program (71111.11) .............................7

1R12 Maintenance Effectiveness (71111.12) .......................................................8

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)..9

1R15 Operability Evaluations (71111.15) ...........................................................10

1R18 Plant Modifications (71111.18) ..................................................................11

1R19 Post-Maintenance Testing (71111.19) ......................................................12

1R20 Outage Activities (71111.20) .....................................................................13

1R22 Surveillance Testing (71111.22)................................................................15

1EP6 Drill Evaluation (71114.06) ........................................................................18

2. Radiation SAFETY ........19

2OS1 Access Control to Radiologically Significant Areas (71121.01) .................19

2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02) ...22

4OA1 Performance Indicator Verification (71151) ...............................................23

4OA2 Identification and Resolution of Problems (71152)....................................28

4OA5 Other Activities 30

4OA6 Management Meetings ..32

4OA7 Licensee-Identified Violations....................................................................33

SUPPLEMENTAL INFORMATION ..1

Key Points of Contact ..1

List of Items Opened, Closed and Discussed............................................................................1

List of Documents Reviewed ..2

Enclosure

SUMMARY OF FINDINGS

IR 05000454/2008-005, 05000454/2008-005; October 1 - December 31, 2008; Byron Station,

Units 1 & 2; Refueling and Other Outage Activities, and Access Control to Radiologically

Significant Areas.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings were identified by the

inspectors. The findings were considered to be Non-Cited Violations of NRC regulations.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings

for which the SDP does not apply may be Green or be assigned a severity level after NRC

management review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,

dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a finding of very low safety significance and associated

Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, for the licensees failure to follow procedure BAP 1450-1,

Access to Containment. Specifically, the inspectors determined that the licensee failed

to remove loose debris items from Unit 2 containment prior to Mode 4 or to perform an

engineering evaluation per procedure. The licensee entered this issue into the

corrective action program (CAP) as Issue Report (IR) 867171, removed the loose debris,

and completed an evaluation to verify that the containment sump was not adversely

affected.

The finding is more than minor because, if left uncorrected, the issue could have

become a more significant safety concern. The inspectors evaluated the finding using

IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial

Screening and Characterization of Finding, dated January 10, 2008, for the Mitigating

Systems Cornerstone. Since this finding was not a design or qualification deficiency, did

not result in loss of system or train safety function, and was not safety significant due to

external events, this issue is screened as very low safety significance. This finding is

related to the Work Control component of the Human Performance cross-cutting area for

the licensees failure to coordinate work activities and the need for work groups to

coordinate with each other. (H.3(b)) The personnel who left the material in containment

assumed it was acceptable as they had documented the material in a surveillance data

sheet, and the personnel who reviewed the completed data sheet assumed the material

had been or would be removed from containment, and none questioned the potential

impact upon the recirculation sump screens or coordinated with each other to ensure

resolution of the material prior to a mode change. (Section 1R20.b)

Cornerstone: Occupational Radiation Safety

Green. The inspectors identified a finding of very low safety significance and associated

NCV of Technical Specification 5.4.1 for failure to implement procedures required to

evaluate radiological hazards for airborne radioactivity. Specifically, the inspectors

1 Enclosure

identified that the licensee failed to re-start an air sampler on the refuel floor which

provided the only air monitoring system while workers were performing activities in the

area. The corrective actions taken by the licensee included starting the required air

sampler. The issue was entered in the licensees corrective action program as

IR 828767.

The finding is more than minor because it impacted the program and process attribute of

the Occupational Radiation Safety Cornerstone and affected the cornerstone objective of

ensuring adequate protection of worker health and safety from exposure to radiation, in

that the failure to fully evaluate the radiological hazards present in work areas could

result in unplanned exposure to workers. The finding was determined to be of very low

safety significance because it was not an As-Low-As-Is-Reasonably-Achievable

(ALARA) planning issue, there was no overexposure nor potential for overexposure, and

the licensees ability to assess dose was not compromised. This finding was caused by

inadequate self-checking and peer checking. Consequently, the cause of this deficiency

had a cross-cutting aspect in the area of Human Performance. (H.4(a)) Specifically, the

licensee failed to utilize human error prevention techniques commensurate with the risk

of the task. (Section 2OS1.1)

B. Licensee-Identified Violations

Four violations of very low safety significance that were identified by the licensee have

been reviewed by inspectors. Corrective actions planned or taken by the licensee have

been entered into the licensees CAP. These violations and corrective action tracking

numbers are listed in Section 4OA7 of this report.

2 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full power throughout the inspection period with minor exceptions.

Unit 2 operated at or near full power throughout the inspection period with one exception. Unit 2

was in a refueling outage from October 6 through October 24, 2009.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Winter Seasonal Readiness Preparations

a. Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant specific design features and the licensees procedures used

to mitigate or respond to adverse weather conditions. Additionally, the inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR) and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant specific procedures. Cold weather protection, such as

heat tracing and area heaters, was verified to be in operation where applicable. The

inspectors also reviewed corrective action program (CAP) items to verify that the

licensee was identifying adverse weather issues at an appropriate threshold and

entering them into their CAP in accordance with station corrective action procedures.

Specific documents reviewed during this inspection are listed in the Attachment. The

inspectors reviews focused specifically on the following plant systems due to their risk

significance or susceptibility to cold weather issues:

  • Diesel Generator Ventilation; and

This inspection constituted one winter seasonal readiness preparations sample as

defined in IP 71111.01-05.

b. Findings

No findings of significance were identified.

3 Enclosure

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Maintenance;

  • Unit 2 Essential Service Water System Following Refueling Outage; and
  • Unit 1 Train A Diesel Generator While Unit 1 Train B Diesel Generator was Out

of Service.

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders, condition reports, and the impact of ongoing work activities on redundant trains

of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment.

These activities constituted three partial system walkdown samples as defined in

IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Division 12 Switchgear Room (Zone 5.1-1);
  • Division 21 Switchgear Room (Zone 5.6-2);

4 Enclosure

  • Auxiliary Building Elevation 451 (Zone 5.6-1);
  • Auxiliary Building Elevation 426 (Zone 5.1-1);
  • Auxiliary Building Elevation 426 (Zone 5.2-1); and
  • Auxiliary Building Elevation 383 (Zone 11.4-0).

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the Attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP.

These activities constituted six quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings of significance were identified.

.2 Annual Fire Protection Drill Observation (71111.05A)

a. Inspection Scope

On September 14 and 21, 2008, the inspectors observed a fire brigade activation for a

Security Diesel Charger Fire. Based on this observation, the inspectors evaluated the

readiness of the plant fire brigade to fight fires. The inspectors verified that the licensee

staff identified deficiencies; openly discussed them in a self-critical manner at the drill

debrief, and took appropriate corrective actions. Specific attributes evaluated were:

(1) proper wearing of turnout gear and self-contained breathing apparatus; (2) proper

use and layout of fire hoses; (3) employment of appropriate fire fighting techniques;

(4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade

leader communications, command, and control; (6) search for victims and propagation of

the fire into other plant areas; (7) smoke removal operations; (8) utilization of pre

planned strategies; (9) adherence to the pre-planned drill scenario; and (10) drill

objectives. In addition, the inspectors evaluated the fire brigades training qualification

and the licensees self-contained breathing apparatus inspection and maintenance

program. Documents reviewed are listed in the Attachment to this report.

These activities constituted one annual fire protection inspection sample as defined by

IP 71111.05-05.

5 Enclosure

b. Findings

No findings of significance were identified.

1R06 Flooding (71111.06)

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the UFSAR, engineering calculations, and abnormal operating procedures to

identify licensee commitments. The specific documents reviewed are listed in the

Attachment to this report. In addition, the inspectors reviewed licensee drawings to

identify areas and equipment that may be affected by internal flooding caused by the

failure or misalignment of nearby sources of water, such as the fire suppression or the

circulating water systems. The inspectors also reviewed the licensees corrective action

documents with respect to past flood-related items identified in the corrective action

program to verify the adequacy of the corrective actions. The inspectors performed a

walkdown of the following plant area(s) to assess the adequacy of watertight doors and

verify drains and sumps were clear of debris and were operable, and that the licensee

complied with its commitments:

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b. Findings

No findings of significance were identified.

1R07 Annual Heat Sink Performance (71111.07)

.1 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed the licensees testing of Unit 2 Train B Diesel Generator Jacket

Water Heat Exchanger and Unit 2 Train C Reactor Containment Fan Cooler (RCFC)

Heat Exchanger to verify that potential deficiencies did not mask the licensees ability to

detect degraded performance, to identify any common cause issues that had the

potential to increase risk, and to ensure that the licensee was adequately addressing

problems that could result in initiating events that would cause an increase in risk. The

inspectors reviewed the licensees observations as compared against acceptance

criteria, the correlation of scheduled testing and the frequency of testing, and the impact

of instrument inaccuracies on test results. Inspectors also verified that test acceptance

criteria considered differences between test conditions, design conditions, and testing

conditions. Documents reviewed are listed in the Attachment to this report.

6 Enclosure

This annual heat sink performance inspection constituted two samples as defined in

IP 71111.07-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

On November 4, 2008, the inspectors observed a crew of licensed operators in the

plants simulator during licensed operator requalification examinations to verify that

operator performance was adequate, evaluators were identifying and documenting crew

performance problems, and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

.2 Licensed Operator Requalification Program (LORT)

a. Inspection Scope

The inspectors performed an inspection of the licensees LORT test/examination

program for compliance with the stations Systems Approach to Training (SAT) program

which would satisfy the requirements of 10 CFR 55.59(c)(4). The reviewed operating

examination material consisted of six operating tests, each containing two or three

dynamic simulator scenarios per operating test and 36 job performance measures

(JPMs). The written examinations reviewed consisted of six written examinations, each

including a Part A, Plant and Control Systems, and Part B, Administrative

7 Enclosure

Controls/Procedure Limits. The examinations contained approximately 35 questions.

The inspectors reviewed the annual requalification operating test and biennial written

examination material to evaluate general quality, construction, and difficulty level. The

inspectors assessed the level of examination material duplication from week-to-week

during the current year operating test. The examiners assessed the amount of written

examination material duplication from week-to-week for the written examination

administered in 2006. The inspectors reviewed the methodology for developing the

examinations, including the LORT program 2-year sample plan, probabilistic risk

assessment insights, previously identified operator performance deficiencies, and plant

modifications. The documents reviewed during this inspection are listed in the

Attachment.

b. Findings

No findings of significance were identified.

.3 Annual Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of the biennial written examination,

the individual JPM operating tests, and the simulator operating tests, which were

required to be given per 10 CFR 55.59(a)(2)) administered by the licensee from

September 22, 2008, through December 15, 2008, as part of the licensees operator

licensing requalification cycle. These results were compared to the thresholds

established in IMC 0609, Appendix I, Licensed Operator Requalification Significance

Determination Process (SDP)." The evaluations were also performed to determine if the

licensee effectively implemented operator requalification guidelines established in

NUREG-1021, Operator Licensing Examination Standards for Power Reactors, and

Inspection Procedure 71111.11, Licensed Operator Requalification Program. The

documents reviewed during this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

  • Auxiliary Building Ventilation System;
  • Unit 1 Train A Diesel Generator Ventilation Failure; and
  • Unit 2 Train A Diesel Generator Failure to Start During Manual Start Surveillance.

8 Enclosure

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2) or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted three quarterly maintenance effectiveness samples as

defined in IP 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • Unit 0 Component Cooling Heat Exchanger Out of Service while Unit 2 Train B

Diesel Generator was Out Of Service (OOS) and Bus Tie Breaker 12-13 was

open;

  • Shutdown Safety during Core Reload with Essential Service Water System

Return X-Tie Valve & Unit 0 Component Cooling Heat Exchanger OOS

Component Cooling Heat Exchanger was OOS; and

  • Unit 2 Train A Diesel Generator Failure to Start During Manual Start Surveillance.

These activities were selected based on their potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

9 Enclosure

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Documents

reviewed are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted

four samples as defined in IP 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

  • Unit 1 Loose Part Monitoring System Noise;
  • Unit 2 Train B Containment Sump Isolation Valve Motor Degradation; and
  • Unit 1 Train B Diesel Generator Cylinder and Head Indications.

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations, to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted four samples as defined in IP 71111.15-05

b. Findings

No findings of significance were identified.

10 Enclosure

1R18 Plant Modifications (71111.18)

.1 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the following temporary modification:

  • Temporary Line to Connect the Drain Lines of Unit 2 A and D Reactor Coolant

Pump Standpipes.

The inspectors compared the temporary configuration change and associated

10 CFR 50.59 screening and evaluation information against the design basis, the

UFSAR, and the TS, as applicable, to verify that the modification did not affect the

operability or availability of the affected system. The inspectors also compared the

licensees information to operating experience information to ensure that lessons learned

from other utilities had been incorporated into the licensees decision to implement the

temporary modification. The inspectors verified that as applicable that the modifications

operated as expected; modification testing adequately demonstrated continued system

operability, availability, and reliability; and that operation of the modifications did not

impact the operability of any interfacing systems. Lastly, the inspectors discussed the

temporary modification with operations, and engineering personnel to ensure that the

individuals were aware of how extended operation with the temporary modification in

place could impact overall plant performance. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted one temporary modification sample as defined in

IP 71111.18-05.

b. Findings

No findings of significance were identified.

.2 Permanent Plant Modifications

a. Inspection Scope

The following engineering design package was reviewed and selected aspects were

discussed with engineering personnel:

This document and related documentation were reviewed for adequacy of the

associated 10 CFR 50.59 safety evaluation screening, consideration of design

parameters, implementation of the modification, post-modification testing, and relevant

procedures, design, and licensing documents were properly updated. The inspectors

observed ongoing and completed work activities to verify that installation was consistent

with the design control documents. The modification added vent locations to safety

related piping in order to allow the removal of air/voids as necessary such as following

maintenance. Documents reviewed are listed in the Attachment to this report.

11 Enclosure

This inspection constituted one permanent plant modification sample as defined in

IP 71111.18-05.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following post-maintenance (PM) activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

Repair;

  • Unit 2 Charging/Safety Injection System Flow Balance following Outage

Maintenance;

  • Unit 1 Train B Charging Pump Return to Service Following Maintenance;

Verification Test;

  • Work Order (WO) 1171264, Operate Diesel Generator 2A in Local Following

Switch Repair;

  • Relay Actuation Surveillance 2BOSR 3.2.8-632A to Test Valve 2AF004A.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion), and test

documentation was properly evaluated. The inspectors evaluated the activities against

TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted seven post-maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings of significance were identified.

12 Enclosure

1R20 Outage Activities (71111.20)

a. Inspection Scope

The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the

Unit 2 refueling outage (RFO - B2R14), conducted October 6 through October 24, 2008,

that the licensee had appropriately considered risk, industry experience, and previous

site-specific problems in developing and implementing a plan that assured maintenance

of defense-in-depth. During the RFO, the inspectors observed portions of the shutdown

and cooldown processes and monitored licensee controls over the outage activities

listed below. Documents reviewed during the inspection are listed in the Attachment to

this report.

  • Licensee configuration management, including maintenance of defense-in-depth

commensurate with the OSP for key safety functions and compliance with the

applicable TS when taking equipment out-of-service.

  • Implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing.

  • Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error.

  • Controls over the status and configuration of electrical systems to ensure that

TS and OSP requirements were met, and controls over switchyard activities.

  • Controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system.

alternative means for inventory addition, and controls to prevent inventory loss.

  • Controls over activities that could affect reactivity.
  • Refueling activities, including fuel handling.
  • Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the containment to verify that debris had not been left which could

block emergency core cooling system suction strainers, and reactor physics

testing.

  • Licensee identification and resolution of problems related to RFO activities.

This inspection constituted one RFO sample as defined in IP 71111.20-05.

b. Findings

Introduction: The inspectors identified a finding of very low safety significance and an

associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, for the licensees failure to follow Procedure BAP 1450-1, Access to

Containment.

Description: On October 22, 2008, the licensee was in the process of restarting Unit 2

from the refueling outage. The inspectors performed an assessment for loose debris

inside of containment following the licensees completion of their readiness for changing

from Mode 5 to Mode 4. During the assessment, the inspectors identified items that

required removal prior to the change in mode, most of which were of a minor nature.

13 Enclosure

Examples included pieces of duct tape, cable ties, several signs, and some trash.

However, items found on the polar crane and items that had been left to support control

rod drop timing testing were required by procedure either to be removed prior to Mode 4

or to have an engineering analysis to support their presence inside containment in

Mode 4 and above.

In Mode 4 and above, the licensee was required by TS to have the emergency sump

operable and thus containment cleanliness was required. At the time when the

inspectors performed their assessment of containment cleanliness, the licensee was in

Mode 5 but was within hours of making the change to Mode 4. Therefore, at the time of

identification by the inspectors, the items were not a challenge to the TS requirements

but should have been removed in preparation for the mode change. The items left for

the control rod drop testing were evaluated by engineering to be left and found to be

acceptable. However, due to an internal licensee miss-communication, the items on the

polar crane were left in place without an engineering evaluation performed. This

condition was not identified until after Mode 4 was achieved. In addition, the licensees

IR, which documented the items found by the inspectors, stated that items on the polar

crane were removed; when in fact, they were still on the crane.

The items that had been left through the mode change into Mode 4 were subsequently

evaluated by the licensee as being acceptable and not a significant challenge to blocking

the containment recirculation sump screens following a postulated accident. After the

final use of the polar crane, these items were removed. They consisted mainly of work

orders, copies of procedures, and fibrous rope.

Analysis: The inspectors determined that the failure to remove loose debris items from

containment prior to Mode 4 or to perform an engineering evaluation as required by

procedure was a performance deficiency warranting a significance determination. Using

IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated

September 20, 2007; the inspectors concluded that the finding was greater than minor

because, if left uncorrected, the issue could have become a more significant safety

concern. The inspectors evaluated the finding using IMC 0609, Significance

Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and

Characterization of Finding, dated January 10, 2008, for the Mitigating Systems

Cornerstone. Since this finding was not a design or qualification deficiency, did not

result in loss of system or train safety function and was not safety significant due to

external events, it was screened as very low safety significance (Green).

This finding is related to the Work Control component of the Human Performance

cross-cutting area for the licensees failure to coordinate work activities and the need for

work groups to coordinate with each other. The personnel who left the material in

containment assumed it was acceptable as they had documented the material in a

surveillance data sheet and the personnel who reviewed the completed data sheet

assumed the material had been or would be removed from containment and none

questioned the potential impact upon the recirculation sump screens or coordinated with

each other to ensure resolution of the material prior to a mode change. (H.3(b))

Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality shall be prescribed by

procedures and accomplished in accordance to these procedure. Byron Administrative

Procedure BAP 1450-1, Revision 37, Access to Containment, was written in

14 Enclosure

accordance with Appendix B. Step 3.2.1 stated in part that, Tools and Equipment taken

into containment in Modes 1, 2, 3, or 4 will be removed when personnel exit

containment. Engineering evaluation and approval is required to leave materials, tools,

and equipment unattended in containment. Contrary to the above, on

October 22, 2008, the inspectors identified that licensee personnel left material inside of

containment in Mode 5 with the knowledge that the material would remain present in

Mode 4 and Mode 3 and an engineering evaluation had not been performed. Because

this violation was of very low safety significance and was captured in the licensees

corrective action program (IR 835427), it is being treated as a NCV consistent with

Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000455/2008005-01)

The inspectors determined that the licensees subsequent failure to promptly correct the

loose debris left inside of containment even though the items had been entered into the

corrective action system was a performance deficiency. Since this violation was

licensee-identified, the enforcement aspect and its safety significance are described in

Section 4OA7 of this report.

1R22 Surveillance Testing (71111.22)

.1 Routine Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • Unit 2 Train B Diesel Generator 18-month Safety Injection Signal Override Test;
  • Unit 2 Train A Diesel Generator Operability Surveillance; and

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency were

in accordance with TSs, the USAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

15 Enclosure

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers code, and reference values were consistent with the

system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted four routine surveillance testing samples, as defined in

IP 71111.22, Section -05.

b. Findings

No findings of significance were identified.

.2 Inservice Testing (IST) Surveillance

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • Unit 2 Charging/Safety Injection System Flow Balance; and

Isolation Valve Leakage Surveillance.

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine whether: any preconditioning occurred; effects of the testing were

adequately addressed by control room personnel or engineers prior to the

commencement of the testing; acceptance criteria were clearly stated, demonstrated

16 Enclosure

operational readiness, and were consistent with the system design basis; plant

equipment calibration was correct, accurate, and properly documented; as left setpoints

were within required ranges; and the calibration frequency were in accordance with TSs,

the UFSAR, procedures, and applicable commitments; measuring and test equipment

calibration was current; test equipment was used within the required range and

accuracy; applicable prerequisites described in the test procedures were satisfied; test

frequencies met TS requirements to demonstrate operability and reliability; tests were

performed in accordance with the test procedures and other applicable procedures;

jumpers and lifted leads were controlled and restored where used; test data and results

were accurate, complete, within limits, and valid; test equipment was removed after

testing; where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of Mechanical

Engineers Code, and reference values were consistent with the system design basis;

where applicable, test results not meeting acceptance criteria were addressed with an

adequate operability evaluation or the system or component was declared inoperable;

where applicable for safety-related instrument control surveillance tests, reference

setting data were accurately incorporated in the test procedure; where applicable, actual

conditions encountering high resistance electrical contacts were such that the intended

safety function could still be accomplished; prior procedure changes had not provided an

opportunity to identify problems encountered during the performance of the surveillance

or calibration test; equipment was returned to a position or status required to support the

performance of its safety functions; and all problems identified during the testing were

appropriately documented and dispositioned in the corrective action program.

Documents reviewed are listed in the Attachment.

This inspection constituted two inservice inspection samples as defined in Inspection

Procedure 71111.22.

b. Findings

No findings of significance were identified.

.3 Containment Isolation Valve Testing

The inspectors reviewed the test results for the following activity to determine whether

the risk-significant system and equipment were capable of performing their intended

safety function and to verify testing was conducted in accordance with applicable

procedural and TS requirements:

  • Local Leak Rate Test for Containment Isolation Valve 1RY8028.

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine whether: any preconditioning occurred; effects of the testing were

adequately addressed by control room personnel or engineers prior to the

commencement of the testing; acceptance criteria were clearly stated, demonstrated

operational readiness, and were consistent with the system design basis; plant

equipment calibration was correct, accurate, and properly documented; as left setpoints

were within required ranges; and the calibration frequency were in accordance with TSs,

the UFSAR, procedures, and applicable commitments; measuring and test equipment

calibration was current; test equipment was used within the required range and

accuracy; applicable prerequisites described in the test procedures were satisfied; test

17 Enclosure

frequencies met TS requirements to demonstrate operability and reliability; tests were

performed in accordance with the test procedures and other applicable procedures;

jumpers and lifted leads were controlled and restored where used; test data and results

were accurate, complete, within limits, and valid; test equipment was removed after

testing; where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was declared

inoperable; where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished; prior

procedure changes had not provided an opportunity to identify problems encountered

during the performance of the surveillance or calibration test; equipment was returned to

a position or status required to support the performance of its safety functions; and all

problems identified during the testing were appropriately documented and dispositioned

in the CAP. Documents reviewed were listed in the Attachment.

This inspection constituted one containment isolation valve inspection sample as defined

in IP 71111.22-05.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a licensee unannounced off-hour drive-in drill

on November 12, 2008, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities. The

inspectors observed emergency response operations in the Technical Support Center

and Operation Support Center to determine whether the event classification,

notifications, protective action recommendations and associated response activities

were performed in accordance with procedures. The inspectors also attended the

licensee drill critique to compare any inspector-observed weakness with those identified

by the licensee staff in order to evaluate the critique and to verify whether the licensee

staff was properly identifying weaknesses and entering them into the corrective action

program. As part of the inspection, the inspectors reviewed the drill package and other

documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b. Findings

No findings of significance were identified.

18 Enclosure

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Plant Walkdowns and Radiation Work Permit Reviews

a. Inspection Scope

The inspectors reviewed licensee controls and surveys in the following radiologically

significant work areas within radiation areas, high radiation areas, and airborne

radioactivity areas in the plant to determine if radiological controls including surveys,

postings, and barricades were acceptable:

  • Unit 2 Containment Building; and
  • Auxiliary Building.

This inspection supplements the sample reported in Inspection

Report 05000454/2008002; 05000455/2008002.

The inspectors reviewed the radiation work permits (RWPs) and work packages used to

access these areas and other high radiation work areas. The inspectors assessed the

work control instructions and control barriers specified by the licensee. Electronic

dosimeter alarm set points for both integrated dose and dose rate were evaluated for

conformity with survey indications and plant policy. The inspectors interviewed workers

to verify that they were aware of the actions required if their electronic dosimeters

noticeably malfunctioned or alarmed.

This inspection supplements the sample reported in Inspection

Report 05000454/2008002; 05000455/2008002.

The inspectors also reviewed the licensees physical and programmatic controls for

highly activated and/or contaminated materials (non-fuel) stored within the spent fuel

pool or other storage pools. Documents reviewed were listed in the Attachment.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

Introduction: A Green NRC-identified finding of very low safety significance and

associated NCV of TS 5.4.1 was identified for failure to implement procedures required

to evaluate radiological hazards for airborne radioactivity.

Description: The inspectors identified that required air samples were not performed

while workers in the reactor cavity were performing reactor disassembly, during the

refueling outage in October 2008. Additionally, a continuous air sampler was not

operating on the 426 elevation of containment.

Airborne radioactivity surveys verify that the radiological conditions are similar to the

conditions predicted during as-low-as-is-reasonably-achievable (ALARA) Planning.

19 Enclosure

Air samples also validate that the controls specified in the ALARA Plan adequately

protect the workers from unnecessary radiation exposure. The evaluation of the

radiological conditions associated with reactor disassembly was documented in RWP

and ALARA Plan 10008916. The ALARA Plan required continuous air sampling in the

reactor cavity in accordance with licensee Procedure RP-AA-302.Continuous air

sampling involved an air sample system consists of a pump and a filter. The filter is

changed periodically and analyzed for radioactivity deposits. On October 8, 2008, the

filter was removed during the previous shift and not replaced with a new filter. The on-

coming shift assumed that a new air sample filter was replaced and that the air sampler

was returned to service. The on-coming shift allowed work crews to enter the reactor

cavity to perform reactor disassembly activities without validating this assumption.

The inspectors reviewed the corrective actions and ensured that a filter was installed

and the pump was operating before leaving containment. Additionally, the licensee

planned to evaluate the issue and to prescribe long-term actions to prevent recurrence.

Analysis: The inspectors determined that this finding was a performance deficiency

because licensees are required to comply with TS requirements and implement various

radiological control procedures. The inspectors also determined that the deficiency was

reasonably within the licensees ability to foresee and correct. The finding is more than

minor because it is associated with the Occupational Radiation Safety cornerstone

attribute of Program and Process and adversely affects the cornerstone objective of

protecting worker health and safety from exposure to radiation. Specifically, the failure

to perform required air sampling impacted the licensees ability to prevent an unplanned

personnel exposure. The finding was assessed using the Occupational Radiation Safety

SDP. The finding was determined to be of very low safety significance (Green), because

it was not an ALARA planning issue, there was no overexposure or potential for

overexposure, and the licensees ability to assess dose was not compromised.

As described above, this finding was caused by inadequate self-checking and peer

checking. Consequently, the cause of this finding had a cross-cutting aspect in the area

of Human Performance. Specifically, the licensee failed to utilize human error

prevention techniques commensurate with the risk of the task. (H.4(a))Enforcement:

Technical Specification 5.4.1.a. requires that the licensee establish, implement, and

maintain procedures specified in Regulatory Guide 1.33, Revision 2, Appendix A, which

specifies procedure for airborne radiation monitoring and for implementing the ALARA

program. Radiation Protection Procedure RP-AA-401, Operational ALARA Planning

and Controls, Revision 9, outlines the requirements for ALARA Plans and requires that

ALARA plans be developed and implemented. The ALARA Plan that evaluated reactor

disassembly and provided the methods and controls associated with reactor

disassembly activities was documented for RWP 10008916. One of the prescribed

controls included in this ALARA Plan required continuous air sampling in the cavity.

Because this finding is of very low safety significance and has been entered into the

licensees corrective action program as IR 828767, this violation is being treated as an

NCV, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000454/2008005-02; 05000455/2008005-02)

20 Enclosure

.2 Job-In-Progress Reviews

a. Inspection Scope

The inspectors observed the following two jobs that were being performed in radiation

areas, airborne radioactivity areas, or high radiation areas for observation of work

activities that presented the greatest radiological risk to workers:

The inspectors reviewed radiological job requirements for these activities, including

RWP requirements and work procedure requirements and attended ALARA job

briefings.

This inspection supplements the sample reported in Inspection

Report 05000454/2008002; 05000455/2008002.

Job performance was observed with respect to the radiological control requirements to

assess whether radiological conditions in the work area were adequately communicated

to workers through pre-job briefings and postings. The inspectors evaluated the

adequacy of radiological controls, including required radiation, contamination, and

airborne surveys for system breaches; radiation protection job coverage, including any

applicable audio and visual surveillance for remote job coverage; and contamination

controls. Documents reviewed were listed in the Attachment.

This inspection supplements the sample reported in Inspection

Report 05000454/2008002; 05000455/2008002.

b. Findings

No findings of significance were identified.

.3 High Risk Significant, High Dose Rate, High Radiation Area, and Very High Radiation

Area Controls

a. Inspection Scope

The inspectors held discussions with the Radiation Protection Manager concerning high

dose rate, high radiation area and very high radiation area controls and procedures,

including procedural changes that had occurred since the last inspection, in order to

assess whether any procedure modifications substantially reduced the effectiveness and

level of worker protection.

The inspectors discussed with radiation protection supervisors the controls that were in

place for special areas of the plant that had the potential to become very high radiation

areas during certain plant operations. The inspectors assessed if plant operations

required communication beforehand with the radiation protection group, so as to allow

corresponding timely actions to properly post and control the radiation hazards.

Documents reviewed were listed in the Attachment.

21 Enclosure

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.4 Radiation Worker Performance

a. Inspection Scope

The inspectors reviewed radiological problem reports for which the cause of the event

was due to radiation worker errors to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. Problems or

issues with planned or completed corrective actions were discussed with the Radiation

Protection Manager. Documents reviewed were listed in the Attachment.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.5 Radiation Protection Technician Proficiency

a. Inspection Scope

The inspectors reviewed radiological problem reports for which the cause of the event

was radiation protection technician error to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. Documents

reviewed were listed in the Attachment.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

2OS2 As-Low-As-Reasonably-Achievable Planning and Controls (71121.02)

.1 Radiological Work Planning

a. Inspection Scope

The inspectors evaluated the licensees list of work activities ranked by estimated

exposure that were in progress and reviewed the following two work activities of highest

exposure significance:

22 Enclosure

This inspection supplements the sample reported in Inspection

Report 05000454/2008002; 05000455/2008002.

For these two activities, the inspectors reviewed the ALARA work activity evaluations,

exposure estimates, and exposure mitigation requirements in order to verify that the

licensee had established procedures and engineering and work controls that were based

on sound radiation protection principles in order to achieve occupational exposures that

were ALARA. The inspectors also determined if the licensee had reasonably grouped

the radiological work into work activities, based on historical precedence, industry

norms, and/or special circumstances.

This inspection supplements the sample reported in Inspection

Report 05000454/2008002; 05000455/2008002.

Documents reviewed were listed in the Attachment.

b. Findings

No findings of significance were identified.

.2 Radiation Worker Performance

a. Inspection Scope

Radiation worker and radiation protection technician performance was observed during

work activities being performed in radiation areas, airborne radioactivity areas, and high

radiation areas that presented the greatest radiological risk to workers. The inspectors

evaluated whether workers demonstrated the ALARA philosophy by being familiar with

the scope of the work activity and tools to be used, by utilizing ALARA low dose waiting

areas, and by complying with work activity controls. Also, radiation worker training and

skill levels were reviewed to determine if they were sufficient relative to the radiological

hazards and the work involved. Documents reviewed were listed in the Attachment.

This inspection supplements the sample reported in Inspection

Report 05000454/2008002; 05000455/2008002.

b. Findings

No findings of significance were identified.

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index - Emergency AC Power System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Unit 1 and Unit 2 Emergency AC Power System performance indicator

for Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third

quarter 2008. To determine the accuracy of the Performance Indicators (PI) data

reported during those periods, PI definitions and guidance contained in the Nuclear

23 Enclosure

Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 5, were used. The inspectors reviewed the licensees operator

narrative logs, MSPI derivation reports, issue reports, event reports, and NRC Integrated

Inspection Reports for the period of October 2007 through September 2008 to validate

the accuracy of the submittals. The inspectors reviewed the MSPI component risk

coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

NEI guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI emergency AC power system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.2 Mitigating Systems Performance Index - High Pressure Injection Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Unit 1 and Unit 2 High Pressure Injection Systems performance indicator for

Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third

quarter 2008. To determine the accuracy of the PI data reported during those periods,

PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors

reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports,

event reports, and NRC Integrated Inspection Reports for the period of October 2007 to

September 2008 to validate the accuracy of the submittals. The inspectors reviewed the

MSPI component risk coefficient to determine if it had changed by more than 25 percent

in value since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified. Documents reviewed are listed in

the Attachment to this report.

This inspection constituted two MSPI high pressure injection system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

24 Enclosure

.3 Mitigating Systems Performance Index - Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Unit 1 and Unit 2 Heat Removal System performance indicator for Byron Unit 1

and Unit 2 for the period from the fourth quarter 2007 through the third quarter 2008.

To determine the accuracy of the PI data reported during those periods, PI definitions

and guidance contained in the NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the

licensees operator narrative logs, issue reports, event reports, MSPI derivation reports,

and NRC Integrated Inspection Reports for the period of October 2007 through

September 2008 to validate the accuracy of the submittals. The inspectors reviewed the

MSPI component risk coefficient to determine if it had changed by more than 25 percent

in value since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified. Documents reviewed are listed in

the Attachment to this report.

This inspection constituted two MSPI heat removal system samples as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.4 Mitigating Systems Performance Index - Residual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Unit 1 and Unit 2 Residual Heat Removal System performance indicator for

Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third

quarter 2008. To determine the accuracy of the PI data reported during those periods,

PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors

reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports,

event reports, and NRC Integrated Inspection Reports for the period of October 2007

through September 2008 to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted two MSPI residual heat removal system samples as defined

in IP 71151-05.

25 Enclosure

b. Findings

No findings of significance were identified.

.5 Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the Unit 1 and Unit 2 Mitigating Systems

Performance Index - Unit 1 and Unit 2 Cooling Water Systems performance indicator for

Byron Unit 1 and Unit 2 for the period from the fourth quarter 2007 through the third

quarter 2008. To determine the accuracy of the PI data reported during those periods,

PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors

reviewed the licensees operator narrative logs, issue reports, MSPI derivation reports,

event reports, and NRC Integrated Inspection Reports for the period of October 2007

through September 2008 to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable NEI guidance. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted two MSPI cooling water system samples as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.6 Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the Reactor Coolant System (RCS)

Specific Activity performance indicator for the period of June 2007 through August 2008

to determine the accuracy of the PI data reported during those periods, PI definitions

and guidance contained in the NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the

licensees RCS chemistry samples, TS requirements, issue reports, event reports and

NRC Integrated Inspection Reports for the period of June 2007 through August 2008 to

validate the accuracy of the submittals. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. In addition to record

reviews, the inspectors observed a chemistry technician obtain and analyze a reactor

coolant system sample. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two reactor coolant system specific activity samples as

defined in IP 71151-05.

26 Enclosure

b. Findings

No findings of significance were identified.

.7 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Leakage performance indicator

Unit 1 Reactor Coolant System Identified Leakage and Unit 2 Reactor Coolant System

Identified Leakage. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors

reviewed the licensees operator logs, RCS leakage tracking data, issue reports, event

reports, and NRC Integrated Inspection Reports for the period of March 2007 to

November 2008 to validate the accuracy of the submittals. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two reactor coolant system leakage samples as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.8 Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent

Occurrences

a. Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent TS

(RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences

performance indicator for the period of June 2007 through August 2008. The inspectors

used PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5 to determine the accuracy of

the PI data reported during those periods. The inspectors reviewed the licensees issue

report database and selected individual reports generated since this indicator was last

reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or

improperly calculated effluent releases that may have impacted offsite dose. The

inspectors reviewed gaseous effluent summary data and the results of associated offsite

dose calculations for selected dates between June 2007 and August 2008 to determine

if indicator results were accurately reported. The inspectors also reviewed the licensees

methods for quantifying gaseous and liquid effluents and determining effluent dose.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one RETS/ODCM radiological effluent occurrences sample

as defined in IP 71151-05.

27 Enclosure

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of items Entered Into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

28 Enclosure

b. Findings

No findings of significance were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the 6 month period of July 01 through December 31, 2008,

although some examples expanded beyond those dates when the scope of the trend

warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy.

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings of significance were identified.

.4 Selected Issue Follow-Up Inspection: Byron Review of Potential Preconditioning Issue

a. Inspection Scope

During a review of items entered in the licensees CAP, the inspectors observed that the

licensee was following up on potential preconditioning issues identified at Braidwood for

applicability to Byron Station. The inspectors selected this issue for a follow-up

inspection on problem identification and resolution. Documents reviewed are listed in

the Attachment to this report.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings and Observations

In October 2007, the licensee at Braidwood identified a number of potential

preconditioning issues of motor-operated and air-operated valves. Specifically,

preventive maintenance tasks were being performed on the valves prior to the inservice

test such that testing was not being conducted in the as-found condition. Although the

29 Enclosure

ASME Code does not specifically require as-found testing, the NRC had issued several

generic communications on the subject to ensure licensees evaluated the potential

affects of the maintenance on the test results. An action request was initiated to review

this issue for applicability to Byron.

In December 2007, the licensees corporate support group, the licensee and its sister

sites discussed this issue and developed draft guidance on preconditioning. One area

that was considered to be potentially preconditioning was performing stem lubrications

on a valve on the same frequency as the inservice test.

In February 2008, in advance of refueling outage B1R15, the licensee conducted a

review of valves that were tested on a cold shutdown or refueling outage frequency. The

review was performed to determine whether any preventive maintenance was going to

be performed prior to the inservice test on the valve, which could be presumed to be

preconditioning. This review did not identify any instances of preconditioning. The

inspectors, however, questioned six valves that had stem lubrication frequency of once a

refueling cycle and appeared to be performed on the valves prior to the test. This did

not appear to meet the licensees guidance in Procedure ER-AA-302-1006, Generic

Letter 96-05 Program Motor-Operated Valve Maintenance and Testing Guidelines, or

the newly developed draft guidance for what could be potentially considered

preconditioning. The guidance stated that stem lubrication would not be considered

preconditioning unless it was routinely scheduled immediately before and at the same

frequency as the valve test. These six valves appeared to meet the guidance for being

potentially preconditioning issues.

Although the inspectors determined that these valves should have been flagged in the

action request as having potential preconditioning concerns, further review by the

licensee indicated that with the exception of one valve, all the stem lubrications were

performed after the inservice test during the outage. The one exception also had

several other maintenance activities performed during the outage and it was not

conclusive if the testing was performed prior to or after the maintenance. The licensee

indicated that there was not any guidance with respect to the schedule as to whether

testing or maintenance should be performed first. The issue of preconditioning of motor-

operated valves prior to their diagnostic test to meet Generic Letter 96-05, Periodic

Verification of Design-Basis Capability of Safety-Related Power-Operated Valves, may

also be an issue as it may not be possible to verify the valve would have been capable

to operate under design basis conditions for the time frame since the last maintenance

or test without the as-found testing. Although no specific preconditioning issues were

identified, additional scheduling guidance or training may be warranted to highlight the

potential for preconditioning by not testing valves in their as-found condition.

No findings of significance were identified.

.5 4OA5 Other Activities Implementation of Temporary Instruction (TI) 2515/176,

Emergency Diesel Generator Technical Specification Surveillance Requirements

Regarding Endurance and Margin Testing

a. Inspection Scope

The objective of TI 2515/176 was to gather information to assess the adequacy of

nuclear power plant emergency diesel generator endurance and margin testing as

prescribed in plant-specific TS. The inspectors reviewed the licensee's TS, procedures,

30 Enclosure

and calculations, and interviewed licensee personnel to complete the TI. The

information gathered for this TI was forwarded to the Office of Nuclear Reactor

Regulation for further review and evaluation on December 17, 2008. This TI is complete

at Byron Station; however, this TI 2515/176 will not expire until August 31, 2009.

Additional information may be required after review by the Office of Nuclear Reactor

Regulation.

b. Findings

No findings of significance were identified.

.6 Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the INPO plant assessment conducted in

June 2008 and dated December 2008. The inspectors reviewed the report to ensure

that issues identified were consistent with the NRC perspectives of licensee

performance and to verify if any significant safety issues were identified that required

further NRC follow-up.

b. Findings

No findings of significance were identified.

.7 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

  • Multiple tours of operations within the Central and Secondary Security Alarm

Stations;

  • Owner Controlled Area and Protected Area access control posts;
  • Other security officer posts including the ready room and compensatory posts;

and Security equipment log review.

The inspectors also reviewed a report of the results of a survey of the site security

organization relative to its safety conscious work environment. The inspectors

considered whether the surveys were conducted in a manner that encouraged candid

and honest feedback. The results were reviewed to determine whether an adequate

number of staff responded to the survey. The inspectors also reviewed Exelons

self-assessment of the survey results and verified that any issues or areas for

improvement were entered into the corrective action program for resolution.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status review and inspection activities.

31 Enclosure

b. Findings

No findings of significance were identified.

.8 (Closed) Unresolved Items (URI) 05000454/455/2008003-06: Auxiliary Feedwater

Tunnel Hatch Margin to Safety

The licensee had identified that the design analysis for evaluation of the Auxiliary

Feedwater (AFW) tunnel flood seal covers did not include the effects of a high energy

line break in the main steam isolation valve tunnels at another facility. The NRC

inspectors at that facility questioned why a dynamic load factor as a result of the impulse

pressure following a high energy line break had not been considered in an analytic

calculation performed to support the operability evaluation.

Following a review of the licensees evaluation, the inspectors questioned the licensees

conclusion that the operability of the AFW hatches continued to be supported despite

analytical results showing a factor of safety for the concrete expansion anchors

supporting the hatches of less than 2.0, which is contrary to the guidance provided in

NRC Bulletin 79-02, Pipe Support Base Plate Designs Using Concrete Expansion

Anchors. Additionally, the inspectors noted that the licensees evaluation did not

address Section C.13 of NRC Technical Guidance 9900, Operability Determinations &

Functionality Assessment for Resolution of Degraded or Nonconforming Conditions

Adverse to Quality or Safety. Specifically, Section C.13 stated that if a structure was

degraded, the licensee should assess the structures capability of performing its

specified function. As long as the identified degradation did not result in exceeding

acceptance limits specified in applicable design codes and standards referenced in the

design basis documents, the affected structure was either operable or functional. The

licensee also identified additional errors that reduced the margin of safety for the

structural integrity of a high energy line break barrier.

At the close of the inspection period that opened this URI, temporary modifications were

implemented at both facilities that restored the margin of safety to greater than 2.0.

Pending additional follow-up by the inspectors for the past operability and timeliness of

corrective actions, extent of condition, and corrective actions, a URI was opened.

During this inspection period, the issue was assessed by regional inspectors at the other

facility. The inspectors conclusions were reviewed by the inspectors at Byron and

confirmed to be applicable to Byron. The inspectors documented their review in

Section 4OA7 as two licensee-identified violations. This URI is closed.

4OA6 Management Meetings

.1 Exit Meeting Summary

On January 15, 2009, the inspectors presented the inspection results to Mr. D. Hoots

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the material examined during the

inspection was proprietary.

.2 Interim Exit Meetings

32 Enclosure

Interim exits were conducted for:

Areas and Performance Indicator Verification with Mr. D. Hoots, and other

members of the licensees staff on October 10, 2008.

  • Inservice Inspection 71111.08 with Mr. D. Hoots on October 16, 2008. The

inspectors returned proprietary information reviewed during the inspection prior

to leaving the site.

  • TI 2515/176 via telephone with Mr. B. Grundmann and other licensee staff on

November 25, 2008.

  • The licensed operator requalification training written examination and operating

test construction and the biennial written examination and annual operating test

results with Mr. G. Wolfe via telephone on December 15, 2008.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • NRC Order EA-03-009, for Byron Unit 2, requires that the licensee perform

ultrasonic testing of each RPV head penetration nozzle every refueling outage

because of its high susceptibility ranking. Contrary to this, the licensee

discovered during the current B2R14 outage that penetration 41 was not

ultrasonically tested during the prior Unit 2 outage in April 2007 (B2R13). No

observable boric acid deposits were noted as a result of the bare metal visual

examination of the penetration nozzles performed during outages B2R13 and

B2R14; and there were no reportable indications found as a result of the B2R14

ultrasonic test of penetration 41. Based upon this, the violation was of very low

safety significance. The licensee entered this issue into the corrective action

program as IR 829647.

that measures shall be established to assure that conditions adverse to quality,

such as failures, malfunctions, deficiencies, deviations, defective material and

equipment, and non-conformances are promptly identified and corrected.

Licensee Procedure LS-AA-125, Revision 12, Corrective Action Program (CAP)

Procedure, was written in accordance with Criterion XVI. Step 2.12 of

LS-AA-125 requires, in part, a Corrective Action is any action that meets any

of the following. Is necessary to restore a Significance Level 1, 2, or 3

Condition. Contrary to the above, on October 22, 2008, licensee personnel

failed to correct a condition adverse to quality as stated in IR 834410.

Specifically, loose debris that had been left on the polar crane had not been

removed prior to Unit 2 changing from Mode 5 to Mode 4. IR 834410 had been

designated by the licensee as a Significance level 3 condition. This issue is of

very low safety significance because this finding was not a design or qualification

deficiency, did not result in loss of system or train safety function and was not

safety significant due to external events.

33 Enclosure

that measures shall be established to assure that conditions adverse to quality,

such as failures, malfunctions, deficiencies, deviations, defective material and

equipment, and non-conformances are promptly identified and corrected.

Contrary to the above, since April 18, 2007, the licensee failed to promptly

identify and correct conditions adverse to quality regarding design of AFW tunnel

hatch covers. Specifically, upon finding a design deficiency in the hatch

structural calculation, the licensee failed to promptly identify all the related design

issues through more detailed reviews and field inspections, and to complete

corrective actions to address the design deficiencies and to restore the design

margins. This finding was of very low safety significance because the finding did

not represent an actual open pathway in the physical integrity of reactor

containment. The issue was identified in the licensees CAP as IR 857487. The

licensee had completed a temporary modification to increase the safety margin of

the hatches and is in the process of designing a permanent modification to

restore full design margin.

design control measures shall provide for verifying or checking the adequacy of

design, such as by the performance of design reviews, by the use of alternate or

simplified calculation methods, or by the performance of a suitable testing

program. Contrary to this, on December 4, 1987, the licensee failed to ensure

design measures were in place for verifying or checking the adequacy of AFW

hatch cover plate design. Specifically, in Calculation 5.6.3.9, the licensee failed

to ensure that a safety factor in accordance with the station design criteria was

applied in the design of expansion anchors. The issue was identified in the

licensees corrective action as IR 654270. This finding was of very low safety

significance because it did not represent an actual open pathway in the physical

integrity of reactor containment.

ATTACHMENT: SUPPLEMENTAL INFORMATION

34 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Hoots, Site Vice President

W. Grundmann, Regulatory Assurance Manager

Z. Cox, Chemist

G. Contrady, Programs Manager

H. Do, Corporate ISI Engineer

S. Greenlee, Engineering Director

D. Thompson, Radiation Protection Manager

Nuclear Regulatory Commission

R. Skokowski, Branch Chief

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000454/2008005-01 NCV Failure to Remove or Evaluate Loose Debris Inside of

05000455/2008005-01 Containment Prior to Applicable Mode

05000454/2008005-02 NCV Failure to Evaluate Radiological Hazards for Airborne

05000455/2008005-02 Radioactivity

Closed

05000454/2008005-01 NCV Failure to Remove or Evaluate Loose Debris Inside of

05000455/2008005-01 Containment Prior to Applicable Mode

05000454/2008005-02 NCV Failure to Evaluate Radiological Hazards for Airborne

05000455/2008005-02 Radioactivity

05000454; URI Unit 1 and Unit 2 Auxiliary Feedwater Tunnel Hatch Margin

455/2008-003-06 to Safety

1 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection

WO 1020141 01; 89-13 Heat Exchanger Inspection for 2B Diesel Driven AF Pump Closed Cycle

Cooler, October 16, 2008

Issue 846625; Procedure Enhancement, November 18, 2008

BOP SX-T2; SX Tower Operations Guidelines, Revision 12

Section 1R04: Equipment Alignment (Quarterly)

2BOSR 7.8.1-1; Unit 2 Essential Service Water System Valve Position Monthly Surveillance,

Revision 16

BOP DG-1; Diesel Generator Alignment to Standby Condition, Revision 11

BOP VD-5; DG Room Ventilation System Operation, Revision 6

BwOP VD-5; DG Room Ventilation System operation, Revision 12

BwOS VD-1a; Diesel Ventilation Systems; Revision 4

10 CFR 50.59 Screening, BOP Vd-5 DG Room Ventilation System Operation; January 06, 1986

Corrective Action Documents as a Result of NRC Inspection

IR 852537; Compensatory Actions Not Procedurally Directed, December 4, 2008

Section 1R05: Fire Protection (Quarterly)

Corrective Action Documents as a Result of NRC Inspection

IR 842026; Fire Zone Walkdown Issues, November 07, 2008

IR 850920; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

IR 850922; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

IR 850925; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

IR 850926; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

IR 850929; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

IR 850931; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

IR 850932; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

IR 842026; Fire Zone Walkdown Issues, November 07, 2008

IR 847572; Interim NRC Inspector Fire Zone Walkdown Findings, November 20, 2008

Section 1R05: Fire Protection (Annual)

BAP 1100-10; Response Procedure for Fire, Revision 7

BAP 1100-10T1; 401 Fire Brigade Equipment Inventory, Revision 7

Byron Emergency Self-Contained Breathing Apparatus Storage Locations Monthly Inventory,

September 2008

OP-AA-201-003; Fire Drill Performance, Revision 7

2 Attachment

OP-AA-201-005; Fire Brigade Qualification, Revision 6

OP-AA-201-008; Pre-Fire Plans, Revision 1

RP-BY-1000; Maintenance Care and Inspection of the ISI Viking Self-Contained Breathing

Apparatus (SCBA), Revision 9

Self-Contained Breathing Apparatus Monthly Inspection, September 2008

Byron Station Fire Drill Critique Form, August 24, 2008

Summary Report for Each Shift Reflecting Fire Brigade and HazMat Qualification Status,

October 12, 2008

IR 823253; Safe-Guards Information Slows Fire Response, September 27, 2008

Section 1R07: Heat Sink Performance

WO 1036955; Perform As-Found/As-Left Inspections of 2C RCFC

Issue 830146; Replace RCFC Channel Heads with stainless Steel in B2R15, October 13, 2008

IR 830370; Restricted Tubes in 2C RCFC, Need to Plug, October 13, 2008

IR 829315; 2C RCFC Channel Head Degradation, Divider Plates, October 10, 2008

Section 1R08: Inservice Inspection Activities

IR 829647; Penetration 41 Not Examined During B2R13; October 11, 2008

IR 831084; Foreign Objects Found In 2C SG Secondary Side - B2R14; October 15, 2008

IR 829610; Acceptance Criteria Used On SX Pipe Was Not Appropriate; October 11, 2008

IR 843635, Steam Generator Tube Sheet Inspection Results - B2R14, November 11, 2008

IR 832181; Foreign Objects Found In 2A SG Secondary - B2R14; dated October 17, 2008

IR 830452; B2R14 - Weld Defects Revealed During Radiography Of Repair; October 14, 2008

IT00717275-02; Buildup of Deposits in Steam Generators, NRC IN 2007-37

ER-AP-335-1012; Bare Metal Visual Examination of PWR Vessel Penetration and Nozzle Safe-

Ends; Revision 3

ER-AP-335-040; Evaluation of Eddy Current Data for Steam Generator Tubing; Revision 4

EXE-ISI-11; Liquid Penetrant Examination, Revision 4

EXE-UT-350; Procedure for Acquiring Material Thickness and Weld Contours; Revision 2

EXE-PDI-UT-2; Ultrasonic Examination of Austenitic Piping Welds in Accordance with PDI-UT-

2; Revision 5

EXAE-ISI-8; VT-1 Direct; Revision 1

ER-AP-335-039; Multi-Frequency Eddy Current Data Acquisition of Steam Generator Tubing;

Revision 5

ER-MW-335-1009; Site Specific Performance; Revision 4

ER-AP-331; Boric Acid Corrosion Control (BACC) Program; Revision 3

ER-AP-331-1001; Boric Acid Corrosion control (BACC) Inspection Locations, Implementation

and Inspection Guidelines; Revision 3

ER-AP-331-1002; Boric Acid Corrosion control Program Identification, Screening, and

Evaluation; Revision 4

ER-AP-331-1004; Boric Acid Corrosion Control (BACC) Training and Qualification, Revision 2

ER-AP-420-002; Byron/Braidwood Unit 2: Steam Generator Eddy Current Activities; Revision 8

Section 1R11: Licensed Operator Requalification Program

Six Reactor Operator Biennial Written Examinations for CY 2008; no dates

Thirty Senior Reactor Operator Examination Questions for CY 2008 Exams; no dates

Twelve Dynamic Simulator Scenarios; no dates

3 Attachment

48 Job Performance Measures; no dates

Licensed Operator Written Examination and Operating Test Results, CY 2008; no date

Section 1R12: Maintenance Effectiveness

IR 417274; Hydramotor Indication Shows Open but Damper Blades are Closed, March 11, 2002

IR 460411; VA Supply/Exhaust Fan Vibration Alarm Setpoint Basis Concern

IR 717005; VA-Tolerance for Equipment Degradation, January 1, 2008

IR 726481; High Vibrations on 0C VA Fan (Supply Fan), January 24, 2008

IR 727128; VA Issues, January 26, 2008

IR 735812; VA Concerns, February 13, 2001

IR 748406; Need (A)(1) Determination: VA Unacceptable Performance Trend, March 12, 2008

IR 850742; Control Damper Problems for 1A DG Ventilation, December 01, 2008

IR 869580; MM Expanded Scope Replace Linear Converter, January 23, 2007

IR 999934; Replace Linear Converter, November 07, 2008

WO 99270872; 1A DG Vent Outside Damp Not Fully Closed, September 13, 2008

VA Degradation/Status Presentations to the Plant Health Committee, December 10, 2007,

February 4, 2008, and May 5, 2008

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Unit 1 Risk Configurations; Week of October 13, 2008, Revision 3

Unit 2 Risk Configurations; Week of November 17, 2008

Protected Equipment Log for 2B DG Outage, October 11, 2008

Protected Equipment Log for Line 0622/Bus 12 Outage, October 12, 2008

Protected Equipment Log for Unit 0 Component Cooling Water Heat Exchanger,

October 11, 2008

Protected Equipment Log for Unit 2 CC Heat Exchanger, November 16, 2008

Protected Equipment Log for 2RA RH Pump Suction OOS, November 17, 2008

B2R14 Shutdown Risk Evaluation; October 15, 2008

B2R14 Outage Status, October 16, 2008

Byron Operations Log; October 15, 2008, to October 16, 2008

OU-AP-104; Shutdown Safety Management Program Byron/Braidwood Annex, Revision 11

IR 832167; NOS Identified OPS Lacks Sensitivity to OLR/SDR, October 17, 2008

Unit 0/1/2 Standing Order; Operator Ownership During IMD Surveillances, October 17, 2008

IR 829481; NOS ID Shutdown Risk Vulnerability, October 10, 2008

Section 1R15: Operability Evaluations

IR 810117; Unit 1 LM Indicates Potential Source of Noise as Near 1RC8002D, August 22, 2008

IR 810867; Expansion Tank Overflow When Started and Running, August 26, 2008

IR 814019; Low JW Level in the 1B AF Pump, September 04, 2008

IR 846398; Need Work Order Created to Replace Grease, November 18, 2008

IR 846420; 2SI8811A; Motor Found Degraded Per Inspection Criteria, November 18, 2008

EC 366163; Operations Evaluation 07-005, Unventable Gas Voids in Containment Recirculation

Sump Piping, November 20, 2008

EC 371879; Operations Evaluation 08-007, Gas Void at 2CS009A, November 20, 2008

EC 371965; Operations Evaluation 08-008, 2B AF Pump Jacket Water Overflow, Revision 000

EC 373393; Operations Evaluation 08-010, 1B DG Cylinder and Head Indications,

December 18, 2008

Fluid Analysis Report; Unit 2 AF Cooler, September 24, 2008

4 Attachment

Operational and Technical Decision Making 2008 - 2009; Suspect 1RC8002D Valve guide(s)

Not Properly Retained in Valve Body

Adverse Condition Monitoring and Contingency Plan; Unit 1 Loose Parts Monitoring System

(LPMS) Noise, August 26, 2008

CAE-02-31 Westinghouse Letter; LSIV Loose Parts 50.59 Screen EVAL-02-062, Revision 1,

March 21, 2002

WO 1072112 02; MOV PM, Actuator Inspection, Diagnostic testing, November 18, 2008

Section 1R18: Plant Modifications

IR 842362; 2CV181 2A RCP Standpipe PW Supply Valve Failed to Close, November 08, 2008

IR 843783; Unexpected Alarm, November 12, 2008

IR 846404; Revised Bars for TCP 373002 are Incorrect, November 18, 2008

EC 373002; Installation of Temporary Line to Connect the Drain Lines of RCP Standpipes 2A

and 2D, Revision 0

EC 371360; Install Vent Valve on 2SI05CA-8, Revision 2

EC 373224; Provide Temporary Fans for 1A DG Room, Revision 0

WO 01149077; Install Vent Valve on 2SI05CA-8, October 18, 2008

WO 01149077 13; SEP PMT: VT-2 of 2SI130, October 15, 2008

WO 01149077 14; OP PMT: Verify No Seat leakage on 2SI130, October 15, 2008

WO 01149077 15; SEP PMT: Record Vibe Data 2SI130 at Full Flow Conditions,

October 15, 2008

Section 1R19: Post Maintenance Testing

1BOSR 3.2.8-610B; Unit 1 ESFAS Instrumentation Slave Relay Surveillance and Automatic

Actuation Test (Train B Automatic Safety Injection - K610), Revision 2

2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Emergency Actuation Signal

Verification Test, Revision 4

WO 999110; 1AP12E-A Relay #1-RCF2 for 1VP01CB Operations PMT Partial 1BOSR 3.2.8-

610B, November 25, 2008

2BOSR 3.2.8-632A; ESFAS Instrumentation Slave Relay Surveillance (Train A Auxiliary

Feedwater Actuation - Relays k632, K639, Revision 2

WO 1165207 01; MM-Repair of 2SI8818C During B2R14

WO 1165207 04; EP - Perform Visual Examination of Disassembled Check Valve

WO 1165207 06; Operations PMT - 2SI8818C SLT Per 2BOSR 4.14.1-1

WO 1165207 07; Operations PMT - 2SI8818C CO Per 2BOSR 5.5.8RH.2-2

WO 1020023 01; 2RH25 VT-2 Exam, October 15, 2008

ASME Section XI Repair/Replacement Plan; 2SI8818C (Loop 3 Cold Leg Accumulation

Injection Check Valve, September 29, 2008

BOP CV-19; Switching Charging Pumps, Revision 14

1BOSR 5.5.1-1; Unit 1 RCS Seal Injection Flow Verification Monthly Surveillance, Revision 4

2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4

Section 1R20: Refueling and Outage Activities

Ultrasonic Thickness Calibration Data Sheet; Report Number 2008-707

IR 826879; Calibrate/Repair 2FI-0928A, October 05, 2008

IR 834405; Need B2R15 W/O to Retrieve Rag and Wire From Upender Pit

B2R14 Work Orders Added to Date, October 15, 2008

5 Attachment

List of Work Orders Removed from B2R14 via SCARF Process as of 7:00 am on

October 16, 2008

1BGP 100-2; Plant Startup, Revision 37

1BGP 100-2A1; Reactor Startup, Revision 26

1BGP 100-2TI; Plant Startup Flowchart, Revision 10

1BGP 100-2T3; Reactor Startup Flowchart, Revision 5

1BGP 100-4; Power Descension, Revision 36

1BGP 100-4T1; Power Descension Flowchart, Revision 11

1BGP 100-5; Plant Shutdown and Cooldown, Revision 53

1BGP 100-5TI; Plant Shutdown and Cooldown Flowchart, Revision 26

BOP RH-6; Operation of the RH System in Shutdown Cooling, Revision 36

BOP RH-8; Filling the Refueling Cavity for Refueling, Revision 18

BOP RH-9; Pump Down of the Refueling Cavity to the RWST, Revision 24

ALM Corporation Material Handling Platform Lift Manual

BAP 1450-1; Access to Containment, Revision 37

2BOSR Z.5.B.1-1; Containment Loose Debris Inspection, Revision 0

Issue 834555; B2R14 Reactor Cavity Hoist Cable Ties, October 22, 2008

LS-AA-125; Corrective Action Program Procedure, Revision 12

IR 833539; White Plastic Cable Tie Not Immediately Retrievable, October 20, 2008

IR 834002; Foreign Material in 2B ECCS Recirculation Sump, October 21,2008

IR 834087; Loose Debris Walkdown Items Requiring Disposition, October 21, 2008

IR 835427; B2R14 LL - Weakness in Control of Material Left in Containment, October 23, 2008

EC 372856; Evaluation of Foreign Material in Unit 2 Containment Building, November 12, 2008

Corrective Action Documents as a Result of NRC Inspection

IR 833612; Inactive Boric Acid Leak on 2SI8822C, October 20, 2008

IR 833613; Inactive Boric Acid Leak on 2SI8810C, October 20, 2008

IR 833881; Inactive Boric Acid Leak, System Not Verified At This Time, October 21, 2008

IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008

IR 856813; Operator Missing a Cover During Mode 4 Walkdown, December 16, 2008

IR 856819; 2LL091E Trickle Charge Light Is Out, December 16, 2008

IR 834410; B2R14 NRC Mode 3 Containment Walkdown Identified Items, October 22, 2008

Section 1R22: Surveillance Testing

1BOSR 6.1.1-11; Primary Containment Type C Local Leakage Rate Tests and IST Tests of

Pressurizer Relief System Partial for 1RY8028, Revision 7

2BOSR 7.5.4-2; Unit 2 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance,

Revision 16

2BOSR 7.5.5-2; Unit 2 Train B Auxiliary Feedwater Valve Verification Test, Revision 4

2BOSR 8.1.2-1; Unit 2 A Diesel Generator Operability Surveillance, Revision 21

2BVSR 5.c.2-1; Unit 2 Charging/Safety Injection System Flow Balance, Revision 4

WO 1024422 01; 2B Diesel Generator SI Signal Override Test, October 14, 2008

WO 1028733 01; Reactor Coolant System CheckValve Leakage Surveillance, October 21, 2008

WO 1157684 01; 1CV01PB Group A IST Requirement for CV Pump, November 06, 2008

Byron Inservice Testing Bases Document; Valve EPN 2SI8818A-D, Loop A-D Cold Leg

Accumulator Injection Check Valve

Byron Inservice Testing Bases Document; Valve EPN 2SI8948A, Accumulator Outlet to RC

Loop Second Check Valve

6 Attachment

BOP DG-11; Diesel Generator Startup, Revision 20

BOP DG-12; Diesel Generator Shutdown, Revision 19

Corrective Action Documents as a Result of NRC Inspection

IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 06, 2008

IR 841953; IST Basis Documents for 1/2SI8818A-D Need Updating, November 07, 2008

Section 2OS1: Access Control to Radiologically Significant Areas

RP-AA-460; Controls for High Radiation and Locked High Radiation Areas; Revision 17

RP-AA-460-001; Controls for Very High Radiation Areas; Revision 1

RP-AA-460; Access to Reactor Incore Sump Area; Revision 2

RP- BY-500-1003; Radiological Controls for Handling Items and Hanging Activated Parts in the

Spent Fuel Pool

Radiation Work Permit and Associated ALARA Reviews; RWP 10008926; B2R14 Seal Table -

Rack Disconnect/Maintenance/Eddy Current/Restoration

Radiation Work Permit and Associated ALARA Reviews; RWP 10009830; P-68 Penetrant Test

and Vent Line Inspection

IR 795311; RWP Violations (PC Requirements); dated July 10, 2008

IR 761294; Level 1 Personal Contamination Event; dated 9, 2008

IR 756342; Worker Entered A/D Platform without Electronic Dosimeter; dated March 29, 2008

IR 754696; Worker Locked Out of RCA - Rad Worker Behavior; dated March 26, 2008

IR 756136; PCE: B1R15 Personal Contamination Event; dated March 28, 2008

IR 673712; RP Not Effectively Using Corrective Action Program; dated September 20, 2007

IR 755986; Alpha Survey Documentation Gaps; dated March 27, 2008

IR 756296; RP-AA-460-1001; Not Completed in Timely Manner; dated March 28, 2008

IR 812338; Ni-63 Source Leak Tests Exceed 6-Month Surveillance Frequency; dated

August 22, 2008

Section 1EP6: Drill Evaluation

IR 844467; OSC Minimum Staffing Not Met for Crew D in Drill, November 13, 2008

Byron 2008 Drive-In Drill; Scenario Information

Nuclear Accident Reporting System (NARS) Form; Utility Message No. 2, November 12, 2008

Issue 844467; OSC Minimum Staffing Not Met for During Drill, November 12, 2008

Section 4OA1: Performance Indicator Verification

LS-AA-2090; Monthly Data Elements for NRC Reactor Coolant System (RCS) Specific Activity;

dated July 3, 2007 through September 2, 2008

LS-AA-2100; Monthly Data Elements for NRC Reactor Coolant System Leakage, Revision 5

LS-AA-2150; Monthly Data Elements for RETS/ODCM Radiological Effluent Occurrences; dated

July 10, 2007 through September 10, 2008

MSPI Derivation Report; Unit 1 and Unit 2 High Pressure Injection System Unavailability and

Unreliability Index, February 2008

Operations Log; February 01, 2008 - February 29, 2008

MSPI Derivation Report; Unit 1 and Unit 2 Cooling Water System Unavailability and Unreliability

Index, March 2008

IR 854124; Inconsequential Error identified in March 2008 MSPI Data for SX,

December 09, 2008

7 Attachment

Operations Log; March 01, 2008 - March 31, 2008

MSPI Derivation Report; Unit 1 and Unit 2 Residual Heat Removal System Unavailability and

Unreliability Index, July 2008

Operations Log; July 01, 2008 - July 31, 2008

MSPI Derivation Report; Unit 1 and Heat Removal System Unavailability and Unreliability Index,

October 2007

Operations Log; October 01, 2007 - October 31, 2007

MSPI Derivation Report; Unit 1 and Unit 2 Heat Removal System Unavailability and Unreliability

Index, April 2008

Operations Log; March 01, 2008 - March 31, 2008

Operations Log; October 01, 2007 - October 31, 2007

MSPI Derivation Report; Unit 1 and Unit 2 Emergency AC Power System Unavailability and

Unreliability Index, June 2008

Operations Log, June 01, 2008 - June 30, 2008

Section 4OA2: Identification and Resolution of Problems

IR 642107; IST Program Implementation, June 19, 2007

IR 678543; Possible Pre-Conditioning Issue - IST Testing, October 1, 2007

IR 686518; Byron Review of Braidwood Potential Pre-Conditioning Issue, October 18, 2007

ER-AA-302-1006; Generic Letter 96-05 Program Motor-Operated Valve Maintenance and

Testing Guidelines, Revision 7

Section 4OA5: Other Activities

1BOSR 8.1.14-1; Unit 1A Diesel Generator 24 Hour Endurance Run, Revision 10

1BOSR 8.1.14-2; Unit 1B Diesel Generator 24 Hour Endurance Run, Revision 8

2BOSR 8.1.14-1; Unit 2A Diesel Generator 24 Hour Endurance Run, Revision 10

2BOSR 8.1.14-2; Unit 2B Diesel Generator 24 Hour Endurance Run, Revision 10

Calculation 19-T-5; Diesel Generator Loading During LOOP/LOCA, Revision 6

8 Attachment

LIST OF ACRONYMS USED

AFW Auxiliary Feedwater System

ALARA As Low As Reasonably Achievable

CAP Corrective Action Program

CFR Code of Federal Regulations

JPM Job Performance Measure

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Inspection Report

IR Issue Report

IST Inservice Testing

LORT Licensed Operator Requalification Training

MSPI Mitigating Systems Performance Index

NCV Non-Cited Violation

NEI Nuclear Energy Institute

NRC U.S. Nuclear Regulatory Commission

OOS Out of Service

ODCM Offsite Dose Calculation Manual

OSP Outage Safety Plan

PI Performance Indicator

RCFC Reactor Containment Fan Cooler

RCS Reactor Coolant System

RETS Radiological Effluent Technical Specifications

RWP Radiation Work Permit

SDP Significance Determination Process

TI Temporary Instructions

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

WO Work Order

9 Attachment