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pm Rtcp | pm Rtcp UNITED STATES l | ||
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'o NUCLEAR REGULATORY COMMISSION | |||
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y" REGION 11 n | |||
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,j 101 MARIETTA STREET,tJ.W. | |||
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's ATL ANTA, GEORGI A 30323 | |||
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..... | |||
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l Report Nos.: | |||
l Report Nos.: | 50-369/87-46 and 50-370/87-46 l | ||
i Licensee: Duke Power Company | |||
422 South Church Street | |||
, | |||
Charlotte, NC 28242 | |||
, | |||
Docket Nos.: 50-369 and 50-370 License Nos.: | |||
NPF-9 and NPF-17 Facility Name: McGuire 1 and 2 Inspection Conduc e - | |||
vember 7 1987 - January 13, 1988 Inspector:,, | |||
b M[ | |||
1. Vrde'rs, Senior Re ident Inspector | |||
/Date Signed | |||
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Accompanying Personnel: D Nelson | |||
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Approved by: / | |||
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b dM | |||
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'T. | |||
AT Pfebres, Section | |||
~i e f Cate Signed Division of Reactor Pro ects a | |||
SUMMARY | |||
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Scope: | |||
This special unannounced inspection involved the areas of operations safety verification and sccveillance testing. | |||
Results: | |||
In the areas inspected, one violation involving an inadequate a | |||
surveillance test program which led to inoperable safety related equipmerit was identified. | |||
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8802090571 080204 | 8802090571 080204 l | ||
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PDR o | |||
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REPORT DETAILS | REPORT DETAILS | ||
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t Persons Contacted Licensee Employees | , | ||
t 1. | |||
! *N. McCraw, Compliance Engineer | Persons Contacted Licensee Employees | ||
*T.-McConnell, Plant Manager | |||
*B. Travis, Superintendent of Operations i | |||
*B. Hamilton, Superintendent of Technical Services | |||
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*N. McCraw, Compliance Engineer L | |||
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Other licensee employees contacted included construction craftsmen, | |||
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engineers, technicians, operators, mechanics, security force members, and | |||
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office personnel. | |||
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* Attended exit interview 2. | |||
Exit Interview The inspection scope and findings were summarized on January 4,1988,'with | |||
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identify as proprietary any of the information reviewed by the inspectors during the course of their | , | ||
corrective actions taken relative to the event described in this | those persons indicated in paragraph 1 above. | ||
! A list of meeting attendees is enclosed as attachment 2. A copy of the | |||
The licensee representatives present offered no dissenting comments nor did they | |||
On November 7,1987, McGuire Unit 2 was restarted from a trip which occurred on November 5. Details of the trip are delineated in inspection report 50-369,370/87-41. At the time of the restart, based on the current test acceptance criteria, both trains of component cooling water (KC) i l | ; | ||
would have failed the test due to fouling of the system | identify as proprietary any of the information reviewed by the inspectors | ||
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during the course of their inspection. | |||
Subsequently, a management nveting was held in the NRC Region II offices on January 13, 1988, at the request of the licensee. | |||
In'that meeting, the licensee explained the background behind, the scenario leading to, and | |||
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corrective actions taken relative to the event described in this report. | |||
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A list of meeting attendees is enclosed as attachment 2. | |||
A copy of the handout issued by the licensee during the meeting is enclosed as Attachment 3. | |||
3. | |||
Unresolved Items No unresolved items were identified in this report. | |||
Executive Summary | |||
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On November 7,1987, McGuire Unit 2 was restarted from a trip which occurred on November 5. | |||
Details of the trip are delineated in inspection report 50-369,370/87-41. At the time of the restart, based on the current test acceptance criteria, both trains of component cooling water (KC) | |||
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would have failed the test due to fouling of the system heat exchangers. | |||
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The heat exchanger fouling was verified later when the Unit 2 KC heat exchangers were tested and failed to meet the test acceptance criteria. | |||
This testing was devised to detect fouling of the tube side of these | |||
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components which is cooled by nuclear service water (RN), a raw lake water system. Testing of these particular heat exchangers is an element of a comprehensive test program implemented in early 1986 as a result of operability concerns involving the fouling of various components in the RN ! | ... | ||
. | |||
components which is cooled by nuclear service water (RN), a raw lake water system. | |||
Testing of these particular heat exchangers is an element of a comprehensive test program implemented in early 1986 as a result of operability concerns involving the fouling of various components in the RN | |||
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system. | |||
This test program incorporated flow balance testing and heat exchanger testing along with heat exchanger cleaning. | |||
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Of concern are the following: | Of concern are the following: | ||
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a. | |||
The effectiveness of the testing program. | |||
b. | |||
The restart of Unit 2 with both trains of KC inoperable, which in turn made both trains of the residual heat removal system (NO) | |||
inoperable. | |||
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c. | |||
The decision to restart the unit when it appears there was ample evidence available prior to restart to challenge the operability of the KC system. | |||
5. | |||
Background In October 1985, a problem was identified concerning the fouling of heat exchangers cooled by Nuclear Service Water (RN). | |||
For more detail relative to the generic issue refer to report 50-369/85-38, 50-370/85-39. Stemming | |||
1 from that problem, which ultimately resulted in escalated enforcement, the licensee implemented an extensive heat exchanger testing program which | |||
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i encompassed the KC heat exchangers. | |||
i As illustrated on page 2 of Attachment 1, a plot of the McGuire Unit 2 KC i | |||
heat exchanger test data for 1986 and 1987, there was at least one i | |||
occurrence in the fall of 1986 and two in the fall of 1987 prior to the | |||
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November 7 event, during which both trains of KC appear to have been l | |||
inoperable simultaneously. | |||
Furthermore, if the Unit 1 KC heat exchanger | |||
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test results are included in the analysis, there were five failures out of the six tests performed between September 4 and October 9, 1987. | |||
6. | |||
Event Scenario l | |||
During a routine staff meeting on the morning of November 4, 1987, licensee management discussed the fact that the Unit 2 KC heat exchanger i | |||
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tests were due cn Friday, November 6 on the A train and on Monday, | |||
tests were due cn Friday, November 6 on the A train and on Monday, | ' | ||
November 9 on B train, j | |||
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On the following morning, November 5,1987, at about 7:00 a.m., Unit 2 tripped from full power due to a loss of vacuum in the main feedwater pump | On the following morning, November 5,1987, at about 7:00 a.m., Unit 2 tripped from full power due to a loss of vacuum in the main feedwater pump | ||
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morning during a routine staff meeting, licensee management again discussed the scheduled KC tests and the probability that the heat exchangers would need to be cleaned when tested, | turbine condensers (Details in report 50-369,370/87-41). | ||
Later that l | |||
morning during a routine staff meeting, licensee management again discussed the scheduled KC tests and the probability that the heat exchangers would need to be cleaned when tested, i | |||
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Neither heat exchanger was tested until Saturday, November 7 after the unit had been restarted. It is of particular interest here to note that had the test been perforrred as scheduled on Friday, November 6 the heat exchanger would have failed. This statement is made based on the test results illustrated on Attachment 1. This would have precluded unit restart in that Technical Specification 3.0.4, applicable to the KC system, prevents a unit from changing modes while in the action statement of a The A train KC heat exchanger was tested on Saturday, failed the test, was declared inoperable and subsequently cleaned. The heat exchanger was retested and declared operable on November | Neither heat exchanger was tested until Saturday, November 7 after the unit had been restarted. | ||
It is of particular interest here to note that had the test been perforrred as scheduled on Friday, November 6 the heat exchanger would have failed. | |||
This statement is made based on the test results illustrated on Attachment 1. | |||
This would have precluded unit restart in that Technical Specification 3.0.4, applicable to the KC system, prevents a unit from changing modes while in the action statement of a T.S. | |||
The A train KC heat exchanger was tested on Saturday, failed the test, was declared inoperable and subsequently cleaned. | |||
The heat exchanger was retested and declared operable on November 10. | |||
During the period between November 7 and 10 the operability of the B KC heat exchanger was not considered. | |||
It is routine practice to assume a component is operable if it is within its surveillance period. | |||
This assumption, hcncver, i: predicated upon an adequate surveillance program. | |||
On November 10, after returning the A heat exchanger to service, the B heat exchanger was tested, it also failed,and was cicaned. The component | |||
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was returned to service later that day. | |||
Of concern is an apparent pattern of inoperability of these heat exchangers, and the restart of the unit on November 7, with what appears to be adequate information available prior to the unit restart forecasting the heat exchangers' degradation. This pattern is graphically depicted on Attachment 1. | |||
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7. | |||
KC System Design Basis The Component Cooling System is designed to: | |||
a. | |||
Remove residual and sensible heat from the Reactor Coolant System, via the Residual Heat Removal System, during normal station shutdown and during accident conditions. | |||
b. | |||
Cool the letdown flow to the Chemical and Voluma Control System during power operation. | |||
l c. | |||
Cool the spent fuel pool water, l | |||
d. | |||
provide cooling to dissipate waste heat from various primary station comporents during normal operation and under accident conditions. | |||
8. | |||
KC System Description | |||
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l l | |||
The Corrponent Cooling System for each of the McGuire units normally l | |||
functions as two independent sub-systems and consists basica'.;y of four pumps and two heat exchangers. | |||
l L | l L | ||
| Line 147: | Line 307: | ||
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Cooling water is normally available to all components served by the system, even though one or more or these con:ponents may be individually isolated. Valves actuated by an Engineered Safety Features (ESF) signal are used to provide essential safety equipment with cooling water should it become necessary to place these compenents in service under loss-of-coolant accident | Cooling water is normally available to all components served by the system, even though one or more or these con:ponents may be individually isolated. | ||
Valves actuated by an Engineered Safety Features (ESF) signal are used to provide essential safety equipment with cooling water should it become necessary to place these compenents in service under loss-of-coolant accident conditions. | |||
The component cooling heat exchangers are the shell and straight tube type, Raw *iver water from the Nuclear Se.rvice Water System is circulated through the straight tubes. | |||
During normal Station operation, two pumps and one heat exchanger provide the necessary cooling requirements. | |||
Two pumps and one heat exchanger are adequate for nonnal cooldown, refueling, and in the event of a LOCA. The remaining pumps and heat exchanger serve as a backup. | |||
Some of the more important equipment serviced by the KC system is: | |||
a. | |||
residual heat removal heat exchangers b. | |||
fuel pool cooling heat exchangers c. | |||
letdown heat exchanger d. | |||
excess letdown heat exchanger e, | |||
reactor coolant pump motor bearings and thermal barriers f. | |||
residual heat removal pump mechanical seal heat exchanger 9. | |||
System Safety Evaluation As discussed in the FSAR, sufficient cooling capacity is provided to fulfill all system requirements under normal and accident conditions. | |||
Adequate safety margins are included in the size and number of components to preclude the possibility of a component malfunction adversely affecting operation of ESF equipment. | |||
Active system components considered vital to the operation of the system are redundant. Any single passive failure in the system should not prevent the system from performing its design function. | |||
In consideration of single failure criteria, the Component Cooling System contains separate flow paths to the tuo trains of ESF Features equipment. | |||
Any piping connecting the separate flow paths contain isolation valves in series. | |||
10. | |||
Applicable Regulatory Requirements a. | |||
10 CFR 50, Appendix B, Criterion XI, requires that a test program be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in | |||
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service is identified and performed in accordance with written test | |||
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procedures which incorporate the requirements and acceptance limits | |||
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contained in applicable design documents. | |||
The test program shall | |||
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include, as appropriate, proof tests prior to installation, | |||
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preoperational tests, and operational tests during nuclear power | |||
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plant operation, of. structures, systems, and components. | |||
Test | |||
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results shall be documented and evaluated to assure that test j | |||
requirements have been satisfied, j | |||
b. | |||
: | Technical Specification (TS) 3.7.3 requires that two independent | ||
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component cooling water loops be operable for modes 1, 2, 3, and 4. | |||
the next six hours and cold shutdown within the following 30 | |||
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With only one loop operable, both loops must be restored to an operable status within 72 hours or the unit be in hot standby within | |||
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the next six hours and cold shutdown within the following 30 hours. | |||
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11. Conclusions | 11. Conclusions | ||
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perform satisfactorily in service, was inadequate in that five of the six tests performed between the dates of September 4 and October 9, , | a. | ||
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j | The test program, established to demonstrate that the KC system will | ||
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Detailed below are the dates, components and results of KC heat l exchanger fouling tests conducted between September 4 and November 2S, | I perform satisfactorily in service, was inadequate in that five of the six tests performed between the dates of September 4 and October 9, | ||
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J 1987 failed. | |||
KC Heat Criteria Actual | |||
The test program, by design, was established to | |||
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j maintain system operability. | |||
The repeated test failures of the KC l | |||
heat exchangers is, sufficient to question program adequacy. | |||
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Detailed below are the dates, components and results of KC heat l | |||
exchanger fouling tests conducted between September 4 and November 2S, 1987. | |||
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i Acceptance l | |||
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KC Heat Criteria Actual | |||
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Date Exchan g DELTA P (PSID) DELTAP(PSID1 Results | |||
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Sept. 10 2B .00 Failed i | |||
Sept. 4 2A 8.8 10.00 Failed | |||
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' | Sept. 10 2B 8.8 10.00 Failed i' | ||
Oct. I 1A 8.8 7.00 Passed | |||
i Test data indicates that both Unit 2 KC heat exchangers were inoperable simultaneously; once during the Fall of 1986 and a number of times during the Fall of 1987, when the unit was operating in modes requiring both trains to be operable, i | ' | ||
Oct. I la 8.8 15.00 Failed Oct. 7 2A 8.8 12.60 Failed I | |||
Oct. 9 | |||
8.8 9.59 Failed | |||
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i Nov. 7 2A 8.8 15.15 Failed | |||
Nov. 10 2B 8.8 20.18 Failed Nov. 25 IB 8.8 14.00 Failed This test data is depicted graphically in Attachment 1. | |||
I l | |||
i b. | |||
Test data indicates that both Unit 2 KC heat exchangers were inoperable simultaneously; once during the Fall of 1986 and a number of times during the Fall of 1987, when the unit was operating in modes requiring both trains to be operable, i | |||
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Subsequent licensee analysis revealed however that based on a model l | Subsequent licensee analysis revealed however that based on a model l | ||
assuming uniform depositing of silt on the HX tubes, the limiting DP | |||
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i for design basis heat transfer is 16.0 psid. | |||
for design basis heat transfer is 16.0 psid. Assuming that type of | |||
the Fall of 1987. The licensee's safety analysis is entailed in LER | Assuming that type of debris geometry, only one KC HX (2B) was actually inoperable during | ||
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the Fall of 1987. | |||
The licensee's safety analysis is entailed in LER | |||
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370/87-22. | |||
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The above is identified as a violation (50-370/87-46-01). | The above is identified as a violation (50-370/87-46-01). | ||
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McGUIPsE | |||
CO!JPO!4ENT COOUNG HX ltdi RESULTS | |||
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o, Jan-86 Jun-86 Dec-86 Jun-87 Dec-87 'S | |||
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KC1B ACCEPTANCE CRITERIA 82-'*-*' | |||
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McGUIRE 2 CO!JPONE!4T COOUNG HX TEST RESULTS | McGUIRE 2 CO!JPONE!4T COOUNG HX TEST RESULTS | ||
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KC2B ACCEPTANCE CRITERIA | |||
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f | f ATTACHMENT 2 i | ||
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Duke Management Meeting Attendees January 13, 1988 | Duke Management Meeting Attendees January 13, 1988 i | ||
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Name Oroanization Position | |||
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, | |||
T. Peebles NRC Section Chief Region !! | |||
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W. T. Orders NRC Senior Resident Inspector, McGuire-l M. Thomas NRC TPS, RII i | |||
j C. Hehl NRC Deputy Director, DRP j | |||
M. L. Ernst NRC Deputy Regional Administrator | |||
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A. F. Gibson NRC Director, DRS | |||
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J. E. Synder Duke MNS/ Performance Engineer | |||
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R. L. Gill Duke McGuire Licensing j | |||
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J E. O. McCraw Duke McGuire Compliance Engineer | |||
! | |||
! | |||
M. A. Haller Duke G. O. Tech Service | |||
! | |||
l M. D. McIntosh Duke General Manager - NRC Support | |||
; | |||
B. H. Hamilton Duke Support of Tech Services - MNS i | |||
j Tony L. McConnel Duke Station Manager /MNS j | |||
: | |||
! | |||
! | |||
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: | |||
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- - | |||
- - | |||
.- | |||
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. | |||
- | |||
. | |||
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t INOPERABILITY IN THE FALL OF 1987 | ATTACPMENT 3 f | ||
. | |||
t | |||
: | |||
! | |||
UNIT 2 COMPONENT COOLING SYSTEM (KC) | |||
' | |||
- | |||
, | |||
t INOPERABILITY IN THE FALL OF 1987 | |||
' | |||
i AS A RESULT OF THE McGUIRE NUCLEAR STATION'S NUCLEAR SERVICE WA | |||
AS A RESULT OF THE McGUIRE NUCLEAR STATION'S NUCLEAR SERVICE WA | . | ||
SYSTEM (RN) TEST PROGRAM WE DISCOVERED THAT THE )(bPERASILITY O | |||
; | ; | ||
SYSTEM ( | THE COMPONENT COOLING SYSTEM (KC) CAN NOT BE ESTABLISHED FOR S | ||
; | |||
! | |||
PERIODS OF TIME DURlhG THE LATE FALL OF 1987. | |||
THE PERIOOS IN QUESTION ARE BETWEEN THE MONTHLY SURVElLLANCES BEING CONOUCTED THAT TIME. | |||
i i | |||
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, | |||
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.,. _ | |||
. | |||
. | . | ||
. | |||
~ | |||
AGENDA FOR DISCUSSION | AGENDA FOR DISCUSSION BRIEF STATEMENT OF PURPOSE OF THE NUCLEAR SERVICE | ||
* | |||
BRIEF STATEMENT OF PURPOSE OF THE NUCLEAR SERVICE WATER SYSTEM (RN) AND THE COMPONENT COOLING SYSTEM (KC) | WATER SYSTEM (RN) AND THE COMPONENT COOLING SYSTEM (KC) | ||
DESCRIPTION OF THE NUCLEAR SERVICE WATER SYSTEM | |||
DESCRIPTION OF THE NUCLEAR SERVICE WATER SYSTEM (RN) TEST PROGRAM AT McGUIRE NUCLEAR STATION | * | ||
(RN) TEST PROGRAM AT McGUIRE NUCLEAR STATION DISCUSSION OF "WHAT WE KNEW", ON NOVEMBER 5, 1987 | |||
DISCUSSION OF "WHAT WE KNEW", ON NOVEMBER 5, 1987 | * | ||
DISCUSSION OF ADDITIONAL INCORMATION OBIAiNED AFTER | |||
DISCUSSION OF ADDITIONAL INCORMATION OBIAiNED AFTER NOVEMBER 7, 1987 | * | ||
NOVEMBER 7, 1987 F.cGUIRE NUCLEAR STATION'S IMME,DIATE REACTI0N TO THE | |||
F.cGUIRE NUCLEAR STATION'S IMME,DIATE REACTI0N TO THE | * | ||
, | |||
AD -:i 7 l ONAL INFORMATION | AD -:i 7 l ONAL INFORMATION CHANGES MADE TO THE NUCLEAR SERVICE WATER SYSTEM | ||
* | |||
CHANGES MADE TO THE NUCLEAR SERVICE WATER SYSTEM (RN) TEST PROGRAM AS A RESULT OF THE ADDITIONAL INFORMATION | (RN) TEST PROGRAM AS A RESULT OF THE ADDITIONAL INFORMATION FUTURE PLANS AND ADDITIONAL STUDIES | ||
* | |||
FUTURE PLANS AND ADDITIONAL STUDIES | * | ||
CONCLUSIONS | CONCLUSIONS | ||
_ _ _ . | _ _ _. | ||
-.- | |||
,,._ | |||
-. - | |||
- | |||
. | |||
. | |||
. | . | ||
PURPOSES OF THE NUCLEAR SERVICE WATER SYSTEM (RN) AND THE COMPONENT COOLING WATER SYSTEM (KC) | PURPOSES OF THE NUCLEAR SERVICE WATER SYSTEM (RN) AND THE COMPONENT COOLING WATER SYSTEM (KC) | ||
NUCLEAR SERVICE WATER SYSTEM (RN) THIS SYSTEM | |||
NUCLEAR SERVICE WATER SYSTEM (RN) THIS SYSTEM PROVIDES ASSURED COOLING WATER FOR VARIOUS AUXILIARY SUILDING AND REACTOR BUILDING HEAT EXCHANGERS DURING ALL PHASES OF STATION | * | ||
PROVIDES ASSURED COOLING WATER FOR VARIOUS AUXILIARY SUILDING AND REACTOR BUILDING HEAT EXCHANGERS DURING ALL PHASES OF STATION OPERATION. | |||
EACH UNIT HAS TWO REDUNDANT "ESSENTIAL HEADERS" SERVING TWO TRAINS OF EQUIPMENT NECESSARY FOR SAFE STATION SHUTDOWN, AND A "NON-ESSENTIAL HEADER" SERVING EQUIPMENT NOT REQUIRED FOR SAFE SHUTDOWN. | |||
IN CONJUNCTION WITH THE ULTIMATE HEAT SINK, COMPRISED OF LAKE NORMAN AND THE STANDBY NUCLEAR SERVICE VATER POND, THE NUCLEAR SERVICE WATER SYSTEM (RN) IS DESIGNED TO MEET DESIGN FLOW RATES AND HEADS FOR NORMAL STATION SHUTDOWN NORMALLY OR AS THE RESULT OF A POSTULATED LOCA. | |||
THE SYSTEM IS FURTHER DESIGNED TO TOLERATE A SINGLE FAILURE FOLLOWillG A LOCA, AND/OR SEISMIC EVENT CAUSING A LOSS OF LAKE NORMAN,,AND/OR LOSS OF STATION POWER PLUS OFFSITE POWER (STATION B LACKOUT). | |||
COMPONENT COOLING SYSTEM (KC) | COMPONENT COOLING SYSTEM (KC) | ||
THIS SYSTEM IS DESIGNED TO: REMOVE RESIDUAL AND SENSIBLE HEAT FROM THE REACTOR COOLANT SYSTEM, VIA THE RESIDUAL HEAT REMOVAL SYSTEM, DURING STATION SHUTDOWN, COOL THE LETDOWN FLOW TO THE CHEMICAL S VOLUME CONTROL SYSTEM DURING POWER | * | ||
VARIOUS PRIMARY STATION COMPONENTS DURING NORMAL OPERATION AND ACCIDENT CONDITION . | THIS SYSTEM IS DESIGNED TO: | ||
A. | |||
REMOVE RESIDUAL AND SENSIBLE HEAT FROM THE REACTOR COOLANT SYSTEM, VIA THE RESIDUAL HEAT REMOVAL SYSTEM, DURING STATION SHUTDOWN, 8. | |||
COOL THE LETDOWN FLOW TO THE CHEMICAL S VOLUME CONTROL SYSTEM DURING POWER OPERATION. | |||
C. | |||
COOL THE SPENT FUEL POOL WATER. | |||
D. | |||
PROVIDE COOLING TO DISSIPATE WASTE HEAT FROM' | |||
VARIOUS PRIMARY STATION COMPONENTS DURING NORMAL OPERATION AND ACCIDENT CONDITION. | |||
DESCRIPTION OF THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGER THESE HEAT EXCHANGERS ARE STANDARD ONCE THROUGH, SHELL AND TUBE HEAT EXCHANGERS WITH THE FOLLOWING SPECIFICATIONS: | DESCRIPTION OF THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGER THESE HEAT EXCHANGERS ARE STANDARD ONCE THROUGH, SHELL AND TUBE HEAT EXCHANGERS WITH THE FOLLOWING SPECIFICATIONS: | ||
NUMBER PER UNIT | NUMBER PER UNIT | ||
, | |||
DESIGN PRESSURE, PSIG 150 O | DESIGN PRESSURE, PSIG 150 O | ||
DESIGN TEMPERATURE, F | DESIGN TEMPERATURE, F | ||
200 | |||
. | |||
DESIGN FLOW (SHELL SIDE), LB/HR 2,610,751 DESIGN FLOW (TUBE SIDE), LB/HR 4,97G,600 O | |||
SHELL SIDE INLET TEMP, F | |||
106 O | |||
SHELL SIDE OUTLET TEMP, F | |||
TUBE SIDE INLET TEMP, F | |||
O TUBE SIDE OUTLET TEMP, F | |||
TUBE O.D., INCHES | SHELL SIDE MATERIAL CARBON STEEL TUBE SIDE MATERIAL INHIBIT 3D ADMIRALTY OVERALL HEAT EXCHANGER LENGTH, FT 41.5 OVERAL HEAT EXCHANGER DIA, FT 5.5 TUBE LENGHTH, FT | ||
TUBE O.D., | |||
INCHES | |||
... | |||
5/8 NUMBER OF TUBES PER HEAT EXCHANGER d 10 0 | |||
, | |||
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- | |||
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- | |||
' | ' | ||
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. | . | ||
NUCLEAR SERVICE WATER SYSTEM (RN) TEST PROGRAM AT MCGUlRE NUCLEAR STATION AS A RESULT OF OPERABILITY CONCER.NS INVOLVING THE FOULING OF VARIOUS COMPONENTS IN THE NUCLEAR SERVICE WATER SYSTEM (RN) A COMPREHESIVE TEST PROGRAM WAS IMPLEMENTED FOR THE SYSTEM IN EA | NUCLEAR SERVICE WATER SYSTEM (RN) TEST PROGRAM AT MCGUlRE NUCLEAR STATION AS A RESULT OF OPERABILITY CONCER.NS INVOLVING THE FOULING OF VARIOUS COMPONENTS IN THE NUCLEAR SERVICE WATER SYSTEM (RN) A COMPREHESIVE TEST PROGRAM WAS IMPLEMENTED FOR THE SYSTEM IN EA 1986. | ||
INQUIRIES FROM OTHER STATIONS, it THE MOST COMPREHENSIVE AND AGGRESSIVE PROGRAM IN THE | THIS TEST PROGRAM INCORPORATED FLOW BALANCE TESTING AND HEAT EXCHANGER TESTING WITH AN AGGRESSIVE HEAT EXCHANGER CLEAN PROGRAM AND A PRE-EXISTING PUMP AND VALVE TEST PROGRAM. | ||
THIS PROGRAM, AS CONFIRMED BY OU? SURVEYS AND BY THE MANY INQUIRIES FROM OTHER STATIONS, it THE MOST COMPREHENSIVE AND AGGRESSIVE PROGRAM IN THE COUNTRY. | |||
... | |||
: | |||
--ra | |||
_ _ _ _ _ _ _ _ _ _ - - - - - - - | _ _ _ _ _ _ _ _ _ _ | ||
- - - - - - - | |||
, | , | ||
i | i | ||
. | . | ||
CURRENT NUCLEAR SERVICE WATER TESTING PROGRAM | CURRENT NUCLEAR SERVICE WATER TESTING PROGRAM NUCLEAR SERVICE WATER FLOW BALANCE QUARTERLY SURVEILLANCE | ||
NUCLEAR SERVICE WATER FLOW BALANCE | * | ||
CLEANING ANY TWO OF THE FOLLOWING HEAT EXCHANGERS | |||
QUARTERLY SURVEILLANCE | * | ||
RN/NS, RN/KC, AND RN/KD ON ONE TRAIN REQUIRES A FLOW B/, LANCE WITHIN 7 DAYS (OR WITHIN 7 DAYS AFTER THE UNIT REfURNS TO NCRMAL OPERATION). | |||
CLEANING ANY TWO OF THE FOLLOWING HEAT EXCHANGERS RN/NS, RN/KC, AND RN/KD ON ONE TRAIN REQUIRES A FLOW B/, LANCE WITHIN 7 DAYS (OR WITHIN 7 DAYS AFTER THE UNIT REfURNS TO NCRMAL OPERATION). | |||
PERIODIC CLEANING OF ALL OTHER HEAT EXCHANGERS DOES | |||
* | |||
NOT REQUIRE A NEW FLOW BALANCE. | |||
CONTAINMENT SPRAY (NS) HEAT EXCHANGERS QUARTERLY HEAT BALANCE TEST | |||
* | |||
* | * | ||
STRUCTURAL INTEGRITY TEST BIENNIALLY | STRUCTURAL INTEGRITY TEST BIENNIALLY | ||
* | |||
CLEAN YEARLY OR AS REQUIRED BY TEST RESULTS COMPONENT COOLING (KC) HEAT EXCHANGERS | CLEAN YEARLY OR AS REQUIRED BY TEST RESULTS COMPONENT COOLING (KC) HEAT EXCHANGERS | ||
* | |||
QUARTERLY DIFFERIENTIAL PRESSURE TEST (MONTHLY | |||
QUARTERLY DIFFERIENTIAL PRESSURE TEST (MONTHLY | _ | ||
. | |||
DURING SEPT. - NOV.) | |||
CLEAN AT REFUELING OR AS REQUIRED BY TEST RESULTS | |||
CLEAN AT REFUELING OR AS REQUIRED BY TEST RESULTS | * | ||
i | |||
. -.. | |||
_ _ -- _. | _ | ||
_ -- | |||
_. | |||
, | , | ||
. | |||
OlESEL GENERATOR COOLING WATER (KD) HEAT EXCHANGER | OlESEL GENERATOR COOLING WATER (KD) HEAT EXCHANGER SEMI-ANNUAL HEAT BALANCE TESTINGX | ||
* | |||
SEMI-ANNUAL HEAT BALANCE TESTINGX | CLEAN AS REQUIRED BY TEST RESULTS | ||
* | |||
CLEAN AS REQUIRED BY TEST RESULTS X | X TESTING HAS BEEN SUSPENDED WHILE CONFLICTING RESULTS ARE EVALUATED. | ||
TESTING HAS BEEN SUSPENDED WHILE CONFLICTING RESULTS ARE | |||
IN THE INTERIM THE HEAT EXCHANGERS ARE CLEANED EVERY 6 MONTHS. | |||
NO TESTING PERFORMED | |||
MOTOR COOLERS AND NI Olt COOLERS | |||
PERIODICALLY CLEANED DEPENDENT ON OBSERVED FOULING LEVELS FROM TWO OR MORE SUCCESSIVE CLEANINGS CURRENT NUCLEAR SERVICE WATER TESTING PROGRAM | * | ||
NO TESTING PERFORMED PERIODICALLY CLEANED DEPENDENT ON OBSERVED FOULING | |||
CENTRI FUGAL CHARGING PUMP (NV) OI L/ GEAR COOLERS | * | ||
LEVELS FROM TWO OR MORE SUCCESSIVE CLEANINGS CURRENT NUCLEAR SERVICE WATER TESTING PROGRAM | |||
QUARTERLY DIFFERENTIAL PRESSURE TEST | ... | ||
CENTRI FUGAL CHARGING PUMP (NV) OI L/ GEAR COOLERS QUARTERLY DIFFERENTIAL PRESSURE TEST | |||
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN ONCE PER FUEL | * | ||
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN | |||
SEMI-ANNUAL DIFFERENTIAL PRESSURE TEST | * | ||
ONCE PER FUEL CYCLE. | |||
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN ONCE PER FUEL | |||
CONTROL ROOM VENTILATION (VC/YC) HEAT EXCHANGERS SEMI-ANNUAL DIFFERENTIAL PRESSURE TEST | |||
* | |||
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN | |||
* | |||
ONCE PER FUEL CYCLE. | |||
. | |||
- | |||
_ | |||
- | |||
. | |||
- | |||
. | |||
~ | |||
SPENT FUEL POOL (KF) PUMP AIR HANDLING UNIT QUARTERLY DIFFERENTIAL PRESSURE TEST | |||
* | |||
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN | |||
* | |||
ONCE PER FUEL CYCLE. | |||
CONTAINMENT SPRAY (NS) AND RESIDUAL HEAT REMOVAL'(ND) PUMPS AIR HANDLING UNITS SEMI-ANNUAL DIFFERENTIAL PRESSURE TEST | |||
* | |||
CLEAN AS REQUIRED BY TEST RESULTS | |||
* | |||
i RETEST POLICY RETEST IS REQUIRED AFTER MAINTENANCE WHEN THE | |||
* | |||
COMPONENT WAS DECLARED INOPERABLE DUE TO TESTING. | |||
PERIODIC CLEANINGS AND OPTIONAL CLEANING WILL NOT REQUIRE RETEST BEFORE RETURNING TO SERVICE. | |||
RETEST WILL BE PERFORMED AS SOON AS POSSIBLE TO OBTAIN BASELINE DATA. | |||
. | |||
-- | |||
McGUIRE NUCLEAR STATION | |||
. | . | ||
- | |||
COMPONENT COOUNG HX TEST RESULTS 20 - | |||
20 - | |||
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KC1B Acceptance Criteria | |||
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- - - - | |||
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McGUIRE NUCLEAR STATION COMPONENT COOUNG HX TEST RESULTS 22 - | McGUIRE NUCLEAR STATION COMPONENT COOUNG HX TEST RESULTS 22 - | ||
- - - - | |||
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KC1A | |||
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KC1B Acceptance Criteria l | |||
l | |||
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. | |||
McGUIRE NUCLEAR STATION COMPONENT COOUNG HX TEST RESULTS 20 - | McGUIRE NUCLEAR STATION COMPONENT COOUNG HX TEST RESULTS 20 - | ||
18 - | 18 - | ||
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McGUIRE NUCLEAR STATION COMPONENT COOUNG HX TEST RESULTS | 3 i | ||
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20 - | Dec-85 Ju!-86 Jan-87 Aug-87 Feb-88 O | ||
KC2A | |||
+ | |||
KC2B Acceptance Criteria | |||
. | |||
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- - - - - | |||
. | |||
- | |||
- - - - - - - | |||
- - - - | |||
- | |||
. - | |||
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- - - | |||
- - - - | |||
- -- | |||
------ -- | |||
- | |||
- --- | |||
- | |||
--- | |||
--- - - - - _, - - - - - - - - - - _ _ - | |||
McGUIRE NUCLEAR STATION COMPONENT COOUNG HX TEST RESULTS | |||
- - - | |||
- - - - - - - - | |||
-- | |||
- | |||
20 - | |||
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18 - | 18 - | ||
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- | |||
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+; | |||
MCGUIRE NUCLEAR STATION'S IMMEDIATE REACTION | ' | ||
- | |||
DISCUSSION OF THE NEED OF PROGRAM ENHANCEMENT BETWEEN PERFORMANCE PERSONNEL AND THE SUPERINTENDENT OF TECHNICAL SERVICES | -.,_ g __ _ | ||
- | |||
COMMUNICATION OF RESULTS TO SENIOR STATION MANAGEMENT (SEE DATED PROFS NOTE) | 2-O i | ||
i | |||
DISCUSSION OF TEST FAILURES WITH THE NRC RESIDENT INSPECTORS | , | ||
, | |||
, | |||
, | |||
i Dec-85 Jul-86 Jan-87 Aug-87 Feb-88 O | |||
KC2A | |||
+ | |||
KC2B Acceptance Criteria | |||
- | |||
. | |||
- | |||
. - | |||
. | |||
. | |||
- | |||
-- | |||
MCGUIRE NUCLEAR STATION'S IMMEDIATE REACTION DISCUSSION OF THE NEED OF PROGRAM ENHANCEMENT | |||
* | |||
BETWEEN PERFORMANCE PERSONNEL AND THE SUPERINTENDENT OF TECHNICAL SERVICES COMMUNICATION OF RESULTS TO SENIOR STATION | |||
* | |||
MANAGEMENT (SEE DATED PROFS NOTE) | |||
DISCUSSION OF TEST FAILURES WITH THE NRC RESIDENT | |||
* | |||
INSPECTORS | |||
* | |||
DOUBLING THE SURVEILLANCE FREQUENCY OF THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGER PRESSURE DROP TESTING | DOUBLING THE SURVEILLANCE FREQUENCY OF THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGER PRESSURE DROP TESTING | ||
. =. | |||
_.. | |||
. | |||
. | |||
- | |||
_ | |||
- | |||
- | |||
, | |||
_ | |||
_ _ _ _. -. | |||
- | |||
. | |||
. | |||
. | |||
CHANGES MADE TO THE NUCLEAR SERVICE WATER SYSTEM (RN) TEST PR | |||
* | |||
TEMPORARY INSTRUMENTATION IS BEING INSTALLED TO ALLOW DAILY MONITORING OF COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS. | |||
INSTALLATION WILL BE COMPLETE BY 3/1/88 AND WILL ALLOW A FULL 6 MONTHS OF BASELINE DATA TO BE COLLECTED PRIOR TO THE FALL OF 1988. | |||
ALL "FAILED" SURVEILLANCES IN THE PERFORMANCE TEST | |||
* | |||
PROGRAM WILL RECElVE A FORMAL, DOCUMENTED REVIEW AND l | |||
APPROPRIATE LEVELS OF MANAGEMENT WILL BE INVOLVED.THIS PROGRAM WILL BE IN EFFECT BY 3/1/88. | |||
(SEE DRAFT VERSION) | |||
. | . | ||
; | |||
i | i | ||
_ _ | _ | ||
_ | |||
NCGUIRE NUCLEAR STATION | - | ||
NCGUIRE NUCLEAR STATION Page 3 PERFORMANCE SECTION FAILED SURVEILLANCE TEST' | |||
POST-TEST ENGINEERING ANALYSIS- | POST-TEST ENGINEERING ANALYSIS- | ||
.**...... DRAFT VERSION ********** | |||
. | |||
REV. 4/ 01-11-88 LOGIC DIAGRAM SURVEILLANCE FAILURE v | REV. 4/ 01-11-88 LOGIC DIAGRAM SURVEILLANCE FAILURE v | ||
i v | i v | ||
' | |||
_- | Y | ||
_- | |||
OPERABILITY OF OTHER | COMMON MODE ANALYSIS i | ||
SAFETY-RELATED COMPONENTS | FAILED COMPONENT SECTION 1.0 HISTORY REVIEW SECTION 2.0 FOCUS FOCUS | ||
---------------------- | |||
- - , r-v~--m - | -------------------- | ||
OPERABILITY OF OTHER OPERATIONAL, MAINT., | |||
SAFETY-RELATED COMPONENTS AND SURVEILLANCE HISTORY OF FAILED COMPONENT | |||
, | |||
- | |||
- | |||
, | |||
r-v~--m | |||
- | |||
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-4 | |||
- | |||
. | . | ||
MCGUIRE NUCLEAR STATION | MCGUIRE NUCLEAR STATION Page 3.1 PERFORMANCE SECTION FAILED SURVEILLANCE TEST POST-TEST ENGINEERING ANALYSIS | ||
********** DRAFT VERSION ********** | |||
REV. 4/ 01-11-88 LOGIC DIAGRAM 1.0: COMMON MODE (CM) ANALYSIS DOES CM Y IDENTIFY CN | REV. 4/ 01-11-88 LOGIC DIAGRAM 1.0: COMMON MODE (CM) ANALYSIS DOES CM Y | ||
IDENTIFY CN HAS CM POTENTIAL | |||
E | > _. | ||
MECHANISMS / | |||
> | |||
OCCURRED. | |||
EXIST? | |||
COMPONENTS (1.3) | |||
(1.1) | |||
(1.1/1.2) | |||
Y N | |||
N l | |||
E V | |||
PROVIDE BASIS | |||
< | |||
(1.1/1.3) | |||
V I | V I | ||
GO TO IS IDENTIFY | GO TO 2.0 IS IDENTIFY (ARE) | ||
INOPERABLE < CM | INOPERABLE | ||
COMP'TS N PERABLE? . OEF (1.3) | < | ||
CM COMP. | |||
< | |||
COMPLETE | |||
<- | |||
COMP'TS N | |||
PERABLE? | |||
. | |||
OEF (1.3) | |||
(1.5) | |||
(1.4) | |||
Y OEF: OPERABILITY V | Y OEF: OPERABILITY V | ||
EVALUATION V | EVALUATION V | ||
NOTIFY | FORM f | ||
NOTIFY RECORD NEXT OPS / COMPLIANCE SURVEILLANCE DATE | |||
V PROVIDE Y UFFICIENT | > | ||
(1.5-1.6) | |||
(1.7) | |||
t | V PROVIDE Y | ||
UFFICIENT | |||
V V | < | ||
BASIS | |||
RESCHEDULE NEXT GO TO .< SURVEILLANCE < | < | ||
MARGIN? | |||
. | |||
(1.8) | |||
(1.8) | |||
t | |||
\\ | |||
V V | |||
! | |||
' | |||
RESCHEDULE NEXT GO TO 2.0 | |||
.< | |||
SURVEILLANCE | |||
< | |||
(1.8) | |||
- | |||
__ _ - _ - | __ | ||
_ - _ - | |||
. | . | ||
MCGUIRE NUCLEAR STATION Page PERFORMANCE SECTION FAILED SURVEILLANCE TEST POST-TEST ENGINEERING ANALYSIS | MCGUIRE NUCLEAR STATION Page 3.2 PERFORMANCE SECTION FAILED SURVEILLANCE TEST POST-TEST ENGINEERING ANALYSIS | ||
********** DRAFT VERSION ********** | |||
REV. 4/ 01-1t-88 LOGIC DIAGRAM 2.0: FAILED COMPONENT HISTORY REVIEW COMPLETE PAST | REV. 4/ 01-1t-88 LOGIC DIAGRAM 2.0: FAILED COMPONENT HISTORY REVIEW COMPLETE PAST COMPLETE WR MNT OPERABILITY | ||
> | |||
INDEP'T REVIEW / | HISTORY | ||
-> | |||
A A y y > | PROBLEM REVIEW REVIEW IDENT.? | ||
Y ASSIGN PIR | (2.1) | ||
(2.2.1) | |||
2.2.1 N | |||
N | Y INDEP'T REVIEW / | ||
ASSIGN PIR APPROVAL | |||
< | |||
TO MNT FOR (3.0) | |||
IDENT.? PROBLEM Y IDENT.? | RESOLUTION | ||
. | |||
A A | |||
y y | |||
> | |||
Y ASSIGN PIR OOT TO OPS FOR CAUSE.. | |||
RESOLUTION | |||
. | |||
IDENT.? | |||
(2.2.1) | |||
N V | |||
ROOT DEFINE OPS | |||
- | |||
CAUSE | |||
<._ | |||
OPS | |||
__< | |||
IMPACTS ( | |||
IDENT.? | |||
PROBLEM Y | |||
IDENT.? | |||
.2.3) | |||
(2.2.2) | |||
2.2.2 N | |||
N v | |||
i ASSIGN PIR SURVEILLANCE j | |||
- > _ _. | |||
PER MGT | |||
> | |||
FREQUENCY INPUT REVIEW (2.2.4) | |||
(2.3) | |||
v SEE NEXT PAGE i | |||
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MCGUIRE NUCLEAR STATION | MCGUIRE NUCLEAR STATION Page 3.3 PERFORMANCE SECTION FAILED SURVEILLANCE TEST POST-TEST ENGINEERING ANALYSIS | ||
+++++***** DRAFT VERSION ********** | |||
REV. 4/ 01-11-88 LOGIC DIAGRAM 2.3: SURVEILLANCE / TEST FREQUENCY REVIEW | REV. 4/ 01-11-88 LOGIC DIAGRAM 2.3: SURVEILLANCE / TEST FREQUENCY REVIEW | ||
SHORT TERM | ' | ||
REVIEW | SHORT TERM REPEAT N | ||
2.1.4 | |||
Y | '%* | ||
N HISTORY | |||
> | |||
FAILURE? | |||
> | |||
GTE 25%? | |||
REVIEW (2.3.1.1 (2.3.1.2) | |||
(2.3.1) | |||
Y Y | |||
V | |||
< | |||
< | |||
! | |||
INCR. | |||
SURV.FREQ ? | |||
2.3. (2.3.1.3) | PROVIDE SHORT TERM N | ||
BASIS / | |||
SURV.FREQ ? | |||
>- | |||
APPROVAL | |||
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2.3.1.3 (2.3.1.3) | |||
V Y | V Y | ||
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COMPLETE | ! | ||
COMPLETE ONG TER | |||
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CALCULATIONS | |||
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HISTORY | |||
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(2.3.2.1 | |||
.3) | |||
REVIEW Y | |||
PMPT N | |||
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> | |||
SURV. FREQ. | |||
N-GTE 25%? | |||
INCREASED? | |||
i (2.3.2.3) | |||
2.3.2.4 N | |||
Y V | |||
V | V | ||
' | |||
V INDEP'T | V INDEP'T PROVIDE REVIEW / | ||
APPR'L | < | ||
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BASIS / | |||
APPR'L APPROVAL (3.0) | |||
(2.3.2.4) | |||
, | |||
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- | |||
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.... | |||
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- | |||
- | |||
e FUTURE PLANS AND ADDITIONAL STUDIES THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS WILL | |||
* | |||
BE PERMANENTLY INSTRUMENTED TO ALLOW CONTINUOUS MONITORING OF PRESSURE DROP BY THE PLANT COMPUTER. | |||
BASED ON CONTINUOUS MONITORING OBSERVATIONS THE | |||
* | |||
COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS WILL BE FLUSHED AT EARLY INDICATIONS OF FOULING. | |||
o THE DESIGN ENGINEERING DEPARTMENT HAS BEEN REQUESTED TO CONSIDER VARIOUS ENGINEERING SOLUTIONS TO THE COMPONENT | |||
' | ' | ||
COOLING SYSTEM (KC) HEAT EXCHANGER FOULING PROBLEM. | |||
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CONCLUSIONS | CONCLUSIONS | ||
* | |||
BASED ON THE INFORMATION AVAILABLE ON NOVEMBER 5, 1987, MCGUIRE NUCLEAR STATION TOOK APPROPRIATE ACTION DURING THE RESTART OF UNIT # * | BASED ON THE INFORMATION AVAILABLE ON NOVEMBER 5, 1987, MCGUIRE NUCLEAR STATION TOOK APPROPRIATE ACTION DURING THE RESTART OF UNIT #2. | ||
BASED ON THE INFORMATION AVAI LABLE NOW, THE UNIT 2 COMPONENT COOLING SYSTEM (KC) WAS DEGRADED AND UNABLE TO l PASS ALL ITS ASSOCIATED SURVEILLANCE TESTS FOR PERIODS DURING THE LATE FALL OF | * BASED ON THE INFORMATION AVAI LABLE NOW, THE UNIT 2 COMPONENT COOLING SYSTEM (KC) WAS DEGRADED AND UNABLE TO l | ||
THE MCGUIRE NUCLEAR STATION NUCLEAR SERVICE WATER SYSTEM (RN) TEST PROGRAM, ALTHOUGH THE MOST EXTENSIVE IN THE COUNTRY, WAS INADEQUATE IN REGARDS-TO ITS TREATMENT OF THF. COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS, IN THAT IT COULD NOT DETECT RAPID DEGRADATION DUE TO ACCELERATED | PASS ALL ITS ASSOCIATED SURVEILLANCE TESTS FOR PERIODS DURING THE LATE FALL OF 1987. | ||
MCGUIRE NUCLEAR STATION HAS REACTED APPROPRIATELY AND IN A TIMELY FASHlON TO ACCELERATED FOULING INCIDENTS OCCURRING DURING THE LATE FALL OF | |||
THESE PERIODS WERE BETWEEN THE MONTHLY SURVElLLANCE INTERVALS USED AT THAT TIME. | |||
THE MCGUIRE NUCLEAR STATION NUCLEAR SERVICE WATER SYSTEM | |||
* | |||
(RN) TEST PROGRAM, ALTHOUGH THE MOST EXTENSIVE IN THE COUNTRY, WAS INADEQUATE IN REGARDS-TO ITS TREATMENT OF THF. COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS, IN THAT IT COULD NOT DETECT RAPID DEGRADATION DUE TO ACCELERATED FOULING. | |||
MCGUIRE NUCLEAR STATION HAS REACTED APPROPRIATELY AND IN | |||
* | |||
A TIMELY FASHlON TO ACCELERATED FOULING INCIDENTS OCCURRING DURING THE LATE FALL OF 1987. | |||
PROGRAM ENHANCEMENTS SHOULD PREVENT A REOCCURRENCE OF THIS PROBLEM. | |||
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}} | }} | ||
Latest revision as of 10:10, 11 December 2024
| ML20149D634 | |
| Person / Time | |
|---|---|
| Site: | McGuire, Mcguire |
| Issue date: | 02/04/1988 |
| From: | William Orders, Peebles T NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML20149D602 | List: |
| References | |
| 50-369-87-46, 50-370-87-46, NUDOCS 8802090571 | |
| Download: ML20149D634 (30) | |
Text
_
pm Rtcp UNITED STATES l
g
'o NUCLEAR REGULATORY COMMISSION
'
y" REGION 11 n
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,j 101 MARIETTA STREET,tJ.W.
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's ATL ANTA, GEORGI A 30323
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l Report Nos.:
50-369/87-46 and 50-370/87-46 l
i Licensee: Duke Power Company
422 South Church Street
,
Charlotte, NC 28242
,
Docket Nos.: 50-369 and 50-370 License Nos.:
NPF-9 and NPF-17 Facility Name: McGuire 1 and 2 Inspection Conduc e -
vember 7 1987 - January 13, 1988 Inspector:,,
b M[
1. Vrde'rs, Senior Re ident Inspector
/Date Signed
Accompanying Personnel: D Nelson
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Approved by: /
W/
b dM
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'T.
AT Pfebres, Section
~i e f Cate Signed Division of Reactor Pro ects a
SUMMARY
[
,
Scope:
This special unannounced inspection involved the areas of operations safety verification and sccveillance testing.
Results:
In the areas inspected, one violation involving an inadequate a
surveillance test program which led to inoperable safety related equipmerit was identified.
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8802090571 080204 l
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REPORT DETAILS
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Persons Contacted Licensee Employees
- T.-McConnell, Plant Manager
- B. Travis, Superintendent of Operations i
- B. Hamilton, Superintendent of Technical Services
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- N. McCraw, Compliance Engineer L
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Other licensee employees contacted included construction craftsmen,
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engineers, technicians, operators, mechanics, security force members, and
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office personnel.
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- Attended exit interview 2.
Exit Interview The inspection scope and findings were summarized on January 4,1988,'with
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those persons indicated in paragraph 1 above.
The licensee representatives present offered no dissenting comments nor did they
identify as proprietary any of the information reviewed by the inspectors
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during the course of their inspection.
Subsequently, a management nveting was held in the NRC Region II offices on January 13, 1988, at the request of the licensee.
In'that meeting, the licensee explained the background behind, the scenario leading to, and
!
corrective actions taken relative to the event described in this report.
!
A list of meeting attendees is enclosed as attachment 2.
A copy of the handout issued by the licensee during the meeting is enclosed as Attachment 3.
3.
Unresolved Items No unresolved items were identified in this report.
Executive Summary
!
On November 7,1987, McGuire Unit 2 was restarted from a trip which occurred on November 5.
Details of the trip are delineated in inspection report 50-369,370/87-41. At the time of the restart, based on the current test acceptance criteria, both trains of component cooling water (KC)
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would have failed the test due to fouling of the system heat exchangers.
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The heat exchanger fouling was verified later when the Unit 2 KC heat exchangers were tested and failed to meet the test acceptance criteria.
This testing was devised to detect fouling of the tube side of these
-.
...
.
components which is cooled by nuclear service water (RN), a raw lake water system.
Testing of these particular heat exchangers is an element of a comprehensive test program implemented in early 1986 as a result of operability concerns involving the fouling of various components in the RN
!
system.
This test program incorporated flow balance testing and heat exchanger testing along with heat exchanger cleaning.
{
Of concern are the following:
'
a.
The effectiveness of the testing program.
b.
The restart of Unit 2 with both trains of KC inoperable, which in turn made both trains of the residual heat removal system (NO)
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c.
The decision to restart the unit when it appears there was ample evidence available prior to restart to challenge the operability of the KC system.
5.
Background In October 1985, a problem was identified concerning the fouling of heat exchangers cooled by Nuclear Service Water (RN).
For more detail relative to the generic issue refer to report 50-369/85-38, 50-370/85-39. Stemming
1 from that problem, which ultimately resulted in escalated enforcement, the licensee implemented an extensive heat exchanger testing program which
i encompassed the KC heat exchangers.
i As illustrated on page 2 of Attachment 1, a plot of the McGuire Unit 2 KC i
heat exchanger test data for 1986 and 1987, there was at least one i
occurrence in the fall of 1986 and two in the fall of 1987 prior to the
November 7 event, during which both trains of KC appear to have been l
inoperable simultaneously.
Furthermore, if the Unit 1 KC heat exchanger
'
test results are included in the analysis, there were five failures out of the six tests performed between September 4 and October 9, 1987.
6.
Event Scenario l
During a routine staff meeting on the morning of November 4, 1987, licensee management discussed the fact that the Unit 2 KC heat exchanger i
,
tests were due cn Friday, November 6 on the A train and on Monday,
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November 9 on B train, j
On the following morning, November 5,1987, at about 7:00 a.m., Unit 2 tripped from full power due to a loss of vacuum in the main feedwater pump
turbine condensers (Details in report 50-369,370/87-41).
Later that l
morning during a routine staff meeting, licensee management again discussed the scheduled KC tests and the probability that the heat exchangers would need to be cleaned when tested, i
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Neither heat exchanger was tested until Saturday, November 7 after the unit had been restarted.
It is of particular interest here to note that had the test been perforrred as scheduled on Friday, November 6 the heat exchanger would have failed.
This statement is made based on the test results illustrated on Attachment 1.
This would have precluded unit restart in that Technical Specification 3.0.4, applicable to the KC system, prevents a unit from changing modes while in the action statement of a T.S.
The A train KC heat exchanger was tested on Saturday, failed the test, was declared inoperable and subsequently cleaned.
The heat exchanger was retested and declared operable on November 10.
During the period between November 7 and 10 the operability of the B KC heat exchanger was not considered.
It is routine practice to assume a component is operable if it is within its surveillance period.
This assumption, hcncver, i: predicated upon an adequate surveillance program.
On November 10, after returning the A heat exchanger to service, the B heat exchanger was tested, it also failed,and was cicaned. The component
'
was returned to service later that day.
Of concern is an apparent pattern of inoperability of these heat exchangers, and the restart of the unit on November 7, with what appears to be adequate information available prior to the unit restart forecasting the heat exchangers' degradation. This pattern is graphically depicted on Attachment 1.
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7.
KC System Design Basis The Component Cooling System is designed to:
a.
Remove residual and sensible heat from the Reactor Coolant System, via the Residual Heat Removal System, during normal station shutdown and during accident conditions.
b.
Cool the letdown flow to the Chemical and Voluma Control System during power operation.
l c.
Cool the spent fuel pool water, l
d.
provide cooling to dissipate waste heat from various primary station comporents during normal operation and under accident conditions.
8.
KC System Description
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The Corrponent Cooling System for each of the McGuire units normally l
functions as two independent sub-systems and consists basica'.;y of four pumps and two heat exchangers.
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Cooling water is normally available to all components served by the system, even though one or more or these con:ponents may be individually isolated.
Valves actuated by an Engineered Safety Features (ESF) signal are used to provide essential safety equipment with cooling water should it become necessary to place these compenents in service under loss-of-coolant accident conditions.
The component cooling heat exchangers are the shell and straight tube type, Raw *iver water from the Nuclear Se.rvice Water System is circulated through the straight tubes.
During normal Station operation, two pumps and one heat exchanger provide the necessary cooling requirements.
Two pumps and one heat exchanger are adequate for nonnal cooldown, refueling, and in the event of a LOCA. The remaining pumps and heat exchanger serve as a backup.
Some of the more important equipment serviced by the KC system is:
a.
residual heat removal heat exchangers b.
fuel pool cooling heat exchangers c.
letdown heat exchanger d.
excess letdown heat exchanger e,
reactor coolant pump motor bearings and thermal barriers f.
residual heat removal pump mechanical seal heat exchanger 9.
System Safety Evaluation As discussed in the FSAR, sufficient cooling capacity is provided to fulfill all system requirements under normal and accident conditions.
Adequate safety margins are included in the size and number of components to preclude the possibility of a component malfunction adversely affecting operation of ESF equipment.
Active system components considered vital to the operation of the system are redundant. Any single passive failure in the system should not prevent the system from performing its design function.
In consideration of single failure criteria, the Component Cooling System contains separate flow paths to the tuo trains of ESF Features equipment.
Any piping connecting the separate flow paths contain isolation valves in series.
10.
Applicable Regulatory Requirements a.
10 CFR 50, Appendix B, Criterion XI, requires that a test program be established to assure that all testing required to demonstrate that structures, systems, and components will perform satisfactorily in
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service is identified and performed in accordance with written test
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procedures which incorporate the requirements and acceptance limits
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contained in applicable design documents.
The test program shall
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include, as appropriate, proof tests prior to installation,
preoperational tests, and operational tests during nuclear power
.
plant operation, of. structures, systems, and components.
Test
results shall be documented and evaluated to assure that test j
requirements have been satisfied, j
b.
Technical Specification (TS) 3.7.3 requires that two independent
-
component cooling water loops be operable for modes 1, 2, 3, and 4.
i
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With only one loop operable, both loops must be restored to an operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the unit be in hot standby within
,
the next six hours and cold shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
>
11. Conclusions
)
a.
The test program, established to demonstrate that the KC system will
>
I perform satisfactorily in service, was inadequate in that five of the six tests performed between the dates of September 4 and October 9,
,
J 1987 failed.
The test program, by design, was established to
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j maintain system operability.
The repeated test failures of the KC l
heat exchangers is, sufficient to question program adequacy.
l'
Detailed below are the dates, components and results of KC heat l
exchanger fouling tests conducted between September 4 and November 2S, 1987.
i Acceptance l
KC Heat Criteria Actual
I
)
Date Exchan g DELTA P (PSID) DELTAP(PSID1 Results
.
Sept. 4 2A 8.8 10.00 Failed
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Sept. 10 2B 8.8 10.00 Failed i'
Oct. I 1A 8.8 7.00 Passed
'
Oct. I la 8.8 15.00 Failed Oct. 7 2A 8.8 12.60 Failed I
Oct. 9
8.8 9.59 Failed
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i Nov. 7 2A 8.8 15.15 Failed
Nov. 10 2B 8.8 20.18 Failed Nov. 25 IB 8.8 14.00 Failed This test data is depicted graphically in Attachment 1.
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Test data indicates that both Unit 2 KC heat exchangers were inoperable simultaneously; once during the Fall of 1986 and a number of times during the Fall of 1987, when the unit was operating in modes requiring both trains to be operable, i
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assuming uniform depositing of silt on the HX tubes, the limiting DP
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Assuming that type of debris geometry, only one KC HX (2B) was actually inoperable during
-
the Fall of 1987.
The licensee's safety analysis is entailed in LER
-
370/87-22.
The above is identified as a violation (50-370/87-46-01).
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f ATTACHMENT 2 i
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Duke Management Meeting Attendees January 13, 1988 i
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Name Oroanization Position
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T. Peebles NRC Section Chief Region !!
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W. T. Orders NRC Senior Resident Inspector, McGuire-l M. Thomas NRC TPS, RII i
j C. Hehl NRC Deputy Director, DRP j
M. L. Ernst NRC Deputy Regional Administrator
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A. F. Gibson NRC Director, DRS
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J. E. Synder Duke MNS/ Performance Engineer
R. L. Gill Duke McGuire Licensing j
J E. O. McCraw Duke McGuire Compliance Engineer
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M. A. Haller Duke G. O. Tech Service
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l M. D. McIntosh Duke General Manager - NRC Support
B. H. Hamilton Duke Support of Tech Services - MNS i
j Tony L. McConnel Duke Station Manager /MNS j
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ATTACPMENT 3 f
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UNIT 2 COMPONENT COOLING SYSTEM (KC)
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t INOPERABILITY IN THE FALL OF 1987
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i AS A RESULT OF THE McGUIRE NUCLEAR STATION'S NUCLEAR SERVICE WA
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SYSTEM (RN) TEST PROGRAM WE DISCOVERED THAT THE )(bPERASILITY O
THE COMPONENT COOLING SYSTEM (KC) CAN NOT BE ESTABLISHED FOR S
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PERIODS OF TIME DURlhG THE LATE FALL OF 1987.
THE PERIOOS IN QUESTION ARE BETWEEN THE MONTHLY SURVElLLANCES BEING CONOUCTED THAT TIME.
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AGENDA FOR DISCUSSION BRIEF STATEMENT OF PURPOSE OF THE NUCLEAR SERVICE
WATER SYSTEM (RN) AND THE COMPONENT COOLING SYSTEM (KC)
DESCRIPTION OF THE NUCLEAR SERVICE WATER SYSTEM
(RN) TEST PROGRAM AT McGUIRE NUCLEAR STATION DISCUSSION OF "WHAT WE KNEW", ON NOVEMBER 5, 1987
DISCUSSION OF ADDITIONAL INCORMATION OBIAiNED AFTER
NOVEMBER 7, 1987 F.cGUIRE NUCLEAR STATION'S IMME,DIATE REACTI0N TO THE
,
AD -:i 7 l ONAL INFORMATION CHANGES MADE TO THE NUCLEAR SERVICE WATER SYSTEM
(RN) TEST PROGRAM AS A RESULT OF THE ADDITIONAL INFORMATION FUTURE PLANS AND ADDITIONAL STUDIES
CONCLUSIONS
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PURPOSES OF THE NUCLEAR SERVICE WATER SYSTEM (RN) AND THE COMPONENT COOLING WATER SYSTEM (KC)
NUCLEAR SERVICE WATER SYSTEM (RN) THIS SYSTEM
PROVIDES ASSURED COOLING WATER FOR VARIOUS AUXILIARY SUILDING AND REACTOR BUILDING HEAT EXCHANGERS DURING ALL PHASES OF STATION OPERATION.
EACH UNIT HAS TWO REDUNDANT "ESSENTIAL HEADERS" SERVING TWO TRAINS OF EQUIPMENT NECESSARY FOR SAFE STATION SHUTDOWN, AND A "NON-ESSENTIAL HEADER" SERVING EQUIPMENT NOT REQUIRED FOR SAFE SHUTDOWN.
IN CONJUNCTION WITH THE ULTIMATE HEAT SINK, COMPRISED OF LAKE NORMAN AND THE STANDBY NUCLEAR SERVICE VATER POND, THE NUCLEAR SERVICE WATER SYSTEM (RN) IS DESIGNED TO MEET DESIGN FLOW RATES AND HEADS FOR NORMAL STATION SHUTDOWN NORMALLY OR AS THE RESULT OF A POSTULATED LOCA.
THE SYSTEM IS FURTHER DESIGNED TO TOLERATE A SINGLE FAILURE FOLLOWillG A LOCA, AND/OR SEISMIC EVENT CAUSING A LOSS OF LAKE NORMAN,,AND/OR LOSS OF STATION POWER PLUS OFFSITE POWER (STATION B LACKOUT).
COMPONENT COOLING SYSTEM (KC)
THIS SYSTEM IS DESIGNED TO:
A.
REMOVE RESIDUAL AND SENSIBLE HEAT FROM THE REACTOR COOLANT SYSTEM, VIA THE RESIDUAL HEAT REMOVAL SYSTEM, DURING STATION SHUTDOWN, 8.
COOL THE LETDOWN FLOW TO THE CHEMICAL S VOLUME CONTROL SYSTEM DURING POWER OPERATION.
C.
COOL THE SPENT FUEL POOL WATER.
D.
PROVIDE COOLING TO DISSIPATE WASTE HEAT FROM'
VARIOUS PRIMARY STATION COMPONENTS DURING NORMAL OPERATION AND ACCIDENT CONDITION.
DESCRIPTION OF THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGER THESE HEAT EXCHANGERS ARE STANDARD ONCE THROUGH, SHELL AND TUBE HEAT EXCHANGERS WITH THE FOLLOWING SPECIFICATIONS:
NUMBER PER UNIT
,
DESIGN PRESSURE, PSIG 150 O
DESIGN TEMPERATURE, F
200
.
DESIGN FLOW (SHELL SIDE), LB/HR 2,610,751 DESIGN FLOW (TUBE SIDE), LB/HR 4,97G,600 O
SHELL SIDE INLET TEMP, F
106 O
SHELL SIDE OUTLET TEMP, F
TUBE SIDE INLET TEMP, F
O TUBE SIDE OUTLET TEMP, F
SHELL SIDE MATERIAL CARBON STEEL TUBE SIDE MATERIAL INHIBIT 3D ADMIRALTY OVERALL HEAT EXCHANGER LENGTH, FT 41.5 OVERAL HEAT EXCHANGER DIA, FT 5.5 TUBE LENGHTH, FT
TUBE O.D.,
INCHES
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5/8 NUMBER OF TUBES PER HEAT EXCHANGER d 10 0
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NUCLEAR SERVICE WATER SYSTEM (RN) TEST PROGRAM AT MCGUlRE NUCLEAR STATION AS A RESULT OF OPERABILITY CONCER.NS INVOLVING THE FOULING OF VARIOUS COMPONENTS IN THE NUCLEAR SERVICE WATER SYSTEM (RN) A COMPREHESIVE TEST PROGRAM WAS IMPLEMENTED FOR THE SYSTEM IN EA 1986.
THIS TEST PROGRAM INCORPORATED FLOW BALANCE TESTING AND HEAT EXCHANGER TESTING WITH AN AGGRESSIVE HEAT EXCHANGER CLEAN PROGRAM AND A PRE-EXISTING PUMP AND VALVE TEST PROGRAM.
THIS PROGRAM, AS CONFIRMED BY OU? SURVEYS AND BY THE MANY INQUIRIES FROM OTHER STATIONS, it THE MOST COMPREHENSIVE AND AGGRESSIVE PROGRAM IN THE COUNTRY.
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CURRENT NUCLEAR SERVICE WATER TESTING PROGRAM NUCLEAR SERVICE WATER FLOW BALANCE QUARTERLY SURVEILLANCE
CLEANING ANY TWO OF THE FOLLOWING HEAT EXCHANGERS
RN/NS, RN/KC, AND RN/KD ON ONE TRAIN REQUIRES A FLOW B/, LANCE WITHIN 7 DAYS (OR WITHIN 7 DAYS AFTER THE UNIT REfURNS TO NCRMAL OPERATION).
PERIODIC CLEANING OF ALL OTHER HEAT EXCHANGERS DOES
NOT REQUIRE A NEW FLOW BALANCE.
CONTAINMENT SPRAY (NS) HEAT EXCHANGERS QUARTERLY HEAT BALANCE TEST
STRUCTURAL INTEGRITY TEST BIENNIALLY
CLEAN YEARLY OR AS REQUIRED BY TEST RESULTS COMPONENT COOLING (KC) HEAT EXCHANGERS
QUARTERLY DIFFERIENTIAL PRESSURE TEST (MONTHLY
_
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DURING SEPT. - NOV.)
CLEAN AT REFUELING OR AS REQUIRED BY TEST RESULTS
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OlESEL GENERATOR COOLING WATER (KD) HEAT EXCHANGER SEMI-ANNUAL HEAT BALANCE TESTINGX
CLEAN AS REQUIRED BY TEST RESULTS
X TESTING HAS BEEN SUSPENDED WHILE CONFLICTING RESULTS ARE EVALUATED.
IN THE INTERIM THE HEAT EXCHANGERS ARE CLEANED EVERY 6 MONTHS.
MOTOR COOLERS AND NI Olt COOLERS
NO TESTING PERFORMED PERIODICALLY CLEANED DEPENDENT ON OBSERVED FOULING
LEVELS FROM TWO OR MORE SUCCESSIVE CLEANINGS CURRENT NUCLEAR SERVICE WATER TESTING PROGRAM
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CENTRI FUGAL CHARGING PUMP (NV) OI L/ GEAR COOLERS QUARTERLY DIFFERENTIAL PRESSURE TEST
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN
ONCE PER FUEL CYCLE.
CONTROL ROOM VENTILATION (VC/YC) HEAT EXCHANGERS SEMI-ANNUAL DIFFERENTIAL PRESSURE TEST
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN
ONCE PER FUEL CYCLE.
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SPENT FUEL POOL (KF) PUMP AIR HANDLING UNIT QUARTERLY DIFFERENTIAL PRESSURE TEST
CLEAN AS REQUIRED BY TEST RESULTS BUT NOT LESS THAN
ONCE PER FUEL CYCLE.
CONTAINMENT SPRAY (NS) AND RESIDUAL HEAT REMOVAL'(ND) PUMPS AIR HANDLING UNITS SEMI-ANNUAL DIFFERENTIAL PRESSURE TEST
CLEAN AS REQUIRED BY TEST RESULTS
i RETEST POLICY RETEST IS REQUIRED AFTER MAINTENANCE WHEN THE
COMPONENT WAS DECLARED INOPERABLE DUE TO TESTING.
PERIODIC CLEANINGS AND OPTIONAL CLEANING WILL NOT REQUIRE RETEST BEFORE RETURNING TO SERVICE.
RETEST WILL BE PERFORMED AS SOON AS POSSIBLE TO OBTAIN BASELINE DATA.
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McGUIRE NUCLEAR STATION
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MCGUIRE NUCLEAR STATION'S IMMEDIATE REACTION DISCUSSION OF THE NEED OF PROGRAM ENHANCEMENT
BETWEEN PERFORMANCE PERSONNEL AND THE SUPERINTENDENT OF TECHNICAL SERVICES COMMUNICATION OF RESULTS TO SENIOR STATION
MANAGEMENT (SEE DATED PROFS NOTE)
DISCUSSION OF TEST FAILURES WITH THE NRC RESIDENT
INSPECTORS
DOUBLING THE SURVEILLANCE FREQUENCY OF THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGER PRESSURE DROP TESTING
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CHANGES MADE TO THE NUCLEAR SERVICE WATER SYSTEM (RN) TEST PR
TEMPORARY INSTRUMENTATION IS BEING INSTALLED TO ALLOW DAILY MONITORING OF COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS.
INSTALLATION WILL BE COMPLETE BY 3/1/88 AND WILL ALLOW A FULL 6 MONTHS OF BASELINE DATA TO BE COLLECTED PRIOR TO THE FALL OF 1988.
ALL "FAILED" SURVEILLANCES IN THE PERFORMANCE TEST
PROGRAM WILL RECElVE A FORMAL, DOCUMENTED REVIEW AND l
APPROPRIATE LEVELS OF MANAGEMENT WILL BE INVOLVED.THIS PROGRAM WILL BE IN EFFECT BY 3/1/88.
(SEE DRAFT VERSION)
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NCGUIRE NUCLEAR STATION Page 3 PERFORMANCE SECTION FAILED SURVEILLANCE TEST'
POST-TEST ENGINEERING ANALYSIS-
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REV. 4/ 01-11-88 LOGIC DIAGRAM SURVEILLANCE FAILURE v
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COMMON MODE ANALYSIS i
FAILED COMPONENT SECTION 1.0 HISTORY REVIEW SECTION 2.0 FOCUS FOCUS
OPERABILITY OF OTHER OPERATIONAL, MAINT.,
SAFETY-RELATED COMPONENTS AND SURVEILLANCE HISTORY OF FAILED COMPONENT
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MCGUIRE NUCLEAR STATION Page 3.1 PERFORMANCE SECTION FAILED SURVEILLANCE TEST POST-TEST ENGINEERING ANALYSIS
- DRAFT VERSION **********
REV. 4/ 01-11-88 LOGIC DIAGRAM 1.0: COMMON MODE (CM) ANALYSIS DOES CM Y
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MECHANISMS /
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MCGUIRE NUCLEAR STATION Page 3.2 PERFORMANCE SECTION FAILED SURVEILLANCE TEST POST-TEST ENGINEERING ANALYSIS
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REV. 4/ 01-1t-88 LOGIC DIAGRAM 2.0: FAILED COMPONENT HISTORY REVIEW COMPLETE PAST COMPLETE WR MNT OPERABILITY
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MCGUIRE NUCLEAR STATION Page 3.3 PERFORMANCE SECTION FAILED SURVEILLANCE TEST POST-TEST ENGINEERING ANALYSIS
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REV. 4/ 01-11-88 LOGIC DIAGRAM 2.3: SURVEILLANCE / TEST FREQUENCY REVIEW
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e FUTURE PLANS AND ADDITIONAL STUDIES THE COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS WILL
BE PERMANENTLY INSTRUMENTED TO ALLOW CONTINUOUS MONITORING OF PRESSURE DROP BY THE PLANT COMPUTER.
BASED ON CONTINUOUS MONITORING OBSERVATIONS THE
COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS WILL BE FLUSHED AT EARLY INDICATIONS OF FOULING.
o THE DESIGN ENGINEERING DEPARTMENT HAS BEEN REQUESTED TO CONSIDER VARIOUS ENGINEERING SOLUTIONS TO THE COMPONENT
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COOLING SYSTEM (KC) HEAT EXCHANGER FOULING PROBLEM.
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CONCLUSIONS
BASED ON THE INFORMATION AVAILABLE ON NOVEMBER 5, 1987, MCGUIRE NUCLEAR STATION TOOK APPROPRIATE ACTION DURING THE RESTART OF UNIT #2.
- BASED ON THE INFORMATION AVAI LABLE NOW, THE UNIT 2 COMPONENT COOLING SYSTEM (KC) WAS DEGRADED AND UNABLE TO l
PASS ALL ITS ASSOCIATED SURVEILLANCE TESTS FOR PERIODS DURING THE LATE FALL OF 1987.
THESE PERIODS WERE BETWEEN THE MONTHLY SURVElLLANCE INTERVALS USED AT THAT TIME.
THE MCGUIRE NUCLEAR STATION NUCLEAR SERVICE WATER SYSTEM
(RN) TEST PROGRAM, ALTHOUGH THE MOST EXTENSIVE IN THE COUNTRY, WAS INADEQUATE IN REGARDS-TO ITS TREATMENT OF THF. COMPONENT COOLING SYSTEM (KC) HEAT EXCHANGERS, IN THAT IT COULD NOT DETECT RAPID DEGRADATION DUE TO ACCELERATED FOULING.
MCGUIRE NUCLEAR STATION HAS REACTED APPROPRIATELY AND IN
A TIMELY FASHlON TO ACCELERATED FOULING INCIDENTS OCCURRING DURING THE LATE FALL OF 1987.
PROGRAM ENHANCEMENTS SHOULD PREVENT A REOCCURRENCE OF THIS PROBLEM.
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