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{{#Wiki_filter:- | {{#Wiki_filter:- | ||
fpA | |||
~ | |||
N9N.A,lw,i ucca,_t F..,0PY. | |||
2 NORTHERN 5TATES POWER COMPANY MIN N E A PO LI S. M S N N E GOTA 95404 lkl n.. | |||
A | |||
/ ' 'I | |||
'f ') v March 7, 1978 | |||
< /d [. | |||
a wa 4 v.s m1973 Q Director, Office of Management O | |||
Information & Program Control C3 c/o Distribution Services Branch, DDC, ADM b | |||
U S Nuclear Regulatory Commission Washington, DC 20555 | |||
==Dear Sir:== | ==Dear Sir:== | ||
MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 Monthly Operating Report February 1978 Attached are two copies of the Monthly Operating Report for February, 1978 for the Monticello Nuclear Generating Plant. | MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 Monthly Operating Report February 1978 Attached are two copies of the Monthly Operating Report for February, 1978 for the Monticello Nuclear Generating Plant. | ||
Yours very truly, | Yours very truly, | ||
%. U er$ | |||
L 0 Mayer, PE Manager of Nuclear Support Services IDM/ak cc: Director, IE-III, USNRC (1) | A L 0 Mayer, PE Manager of Nuclear Support Services IDM/ak cc: Director, IE-III, USNRC (1) | ||
(Director, IE, USNRC (c/o DSB) (10) | (Director, IE, USNRC (c/o DSB) (10) | ||
MPCA Attn: J W Ferman 0 | MPCA Attn: J W Ferman 0 | ||
s, t | s, t | ||
l 9212040488 780228 PDR | l 9212040488 780228 780720022 PDR ADOCK 05000263 R | ||
pyg | |||
NARRATIVE SIM4\Rf 0F OPERATING EXPERIENCE DOCKET NO. 50-263 LNIT | NARRATIVE SIM4\\Rf 0F OPERATING EXPERIENCE DOCKET NO. | ||
DATE | 50-263 LNIT 1 | ||
l DATE 3/6/78 00$PLETED BY A. L. Mvrabo TELEPIKNE 612/295-5151, Ext. 239 | |||
?DNTI Febmary 4 | |||
2/2/78 2/3/78 | 2/1/78 to Operated at 100% of rated power. | ||
2/2/78 2/3/78 Orderly shutdown for rod sequence exchange and re-pair / inspection of tonis vacuum breakers. Trued up bearing housings and bearings and adjusted end clear-ance on toms to drywell vacuum breakers "B" and | |||
2/4/78 | " T". Changed out topworks on "A" relief valve due to leak around strainer plug. | ||
2/23/78 | 2/4/78 Operated at approximately 100% of rated power, except to for weekend reductions to perform control rod exercising 2/22/78 and valve testing. | ||
2/24/78 to | 2/23/78 Reactor scram due to low condenser vacuum caused by both circulating water pumps tripping from spurious flood protection circuit signal. | ||
2/24/78 to Operated at 100% of rated power. | |||
2/28/78 Spent Fuel Storage Update Fuel assemblies in the core - 484 Fuel assemblies in the spent fuel storage pool - 616 Licensed spent fuel storage pool capacity - 740 Date of last refueling that can be discharged with present capacity -Oct, 1978 | 2/28/78 Spent Fuel Storage Update Fuel assemblies in the core - 484 Fuel assemblies in the spent fuel storage pool - 616 Licensed spent fuel storage pool capacity - 740 Date of last refueling that can be discharged with present capacity -Oct, 1978 | ||
1 4 | 1 4 | ||
1 l | 1 l | ||
] | ] | ||
DOCKETNO. 50-263 | OPER ATING DATA REPORT i | ||
DOCKETNO. 50-263 DATE 3/1/78 COMPLETED BY. A.MYRA110 i | |||
COMPLETED BY . A.MYRA110 i | TELEPHONE 612/20s.E151 4 | ||
TELEPHONE 612/20s.E151 | .I i | ||
4 | OPERATING STATUS b | ||
.I i | Monticello Notes | ||
: 1. Unit Name: | : 1. Unit Name: | ||
: 2. deportmg Period: | l | ||
: 2. deportmg Period: | |||
: 4. Nameplate Rating (Grun Mhel. | Febmarv | ||
.l. Licenwd Thermal Power (MWI): | |||
l | 1670 569 | ||
: h. If Changes Occur in Capacity Ratine titems Number 3 Through 7) Since Last Report. Gise Reawne | : 4. Nameplate Rating (Grun Mhel. | ||
j | |||
: 9. Power Letel To Which Restricted.lf | : 5. Design Electrical Rating (Net MWel: | ||
i j | 545.4-564 l | ||
: 6. Masimum Dependable Capacity (Gross MWel: | |||
l | 536 7 Masimum Dependahic Capacity (Net MWe): | ||
: h. If Changes Occur in Capacity Ratine titems Number 3 Through 7) Since Last Report. Gise Reawne (Net MWel: | |||
N/A | |||
: 9. Power Letel To Which Restricted.lf Any/A N | |||
i | |||
: 10. Reasons For Restrictions,If Any.: | |||
i j | |||
This Month Yr..to Date Cumulative 1 | |||
672 1.416 5_8,441 1 l | |||
: 11. Hours in Reporting Period l | |||
: 12. Number Of Hours Resetor Was Critical 644.2 1.388.2 46.556 6 1.1. Reactor Resene Shutdown Hours 0.0 0.0 | |||
-940.7 | |||
: 14. Hours Generatm On.Line 630.3 1,374.3 45,151.7 0.0 0.0 0.0 | |||
)- | )- | ||
: 16. Cross Thermal Energy Generated (MWH) | : 15. Unit Resene Shutdown lluurs | ||
} | : 16. Cross Thermal Energy Generated (MWH) 974.500.8 2.207.824.8 75_.862.399.4 | ||
} | |||
: 17. Gruss Electrical Energy Generated (MWH). | |||
334.120_. _,.. | |||
756.750 23.129.440 | |||
: 15. Net Electrical Energy Generated (MWH) 321.696 729'.302 22'.105.676 | |||
~ | |||
4 | 4 | ||
: 19. Unit Senice Factor 93.8% | |||
: 19. Unit Senice Factor | 97.1% | ||
I- | 77.3% | ||
i l | 93.8% | ||
- 97.lf. | |||
I- | |||
: 20. Unit Availabi:ity Facto, | |||
'7.3% | |||
i l | |||
: 21. Unit Capacity Factor IUsing MDC Neti 89.3% | |||
96.1% | |||
70.6% | |||
87 8% | |||
94 4%- | |||
69.4% | |||
. 2.' | |||
Unit Capacity Factor (Using DER Net)- | |||
: 23. Unit Forced Outage Rate 1.6% | |||
-0.7% | |||
7.8% | |||
: 21. Shutdowns Schedukd User Ne.st 6 Monthy(Type Date,and Duration of Each): | : 21. Shutdowns Schedukd User Ne.st 6 Monthy(Type Date,and Duration of Each): | ||
Refueline Outane. October 16. 1978. 40 days | |||
: 25. If Shut Down At End Of Report Period, Estimated Date of Startup: | : 25. If Shut Down At End Of Report Period, Estimated Date of Startup: | ||
: 26. Units in Test Status (Prior to Commercial Operations N/A | N/A | ||
: 26. Units in Test Status (Prior to Commercial Operations N/A Forecast | |||
~ Achieved INITI AL CRITICALITY r | |||
INITIA L ELECTRICITY COMMERCI A L OPER ATION | |||
+ | + | ||
i P857 ) | |||
P857 ) | |||
1 9' | 1 9' | ||
m A_-, | |||
..A-, | |||
...,m | |||
~m.... | |||
..__,a=.,.. | |||
~ | |||
AVER 4CE D ALLY UNIT POWER LEVEL DOCKET NO. | AVER 4CE D ALLY UNIT POWER LEVEL 50-263 DOCKET NO. | ||
3,IT | i hbnticello 3,IT DATE 3/1/78 COMPLETED fiY A. hhRABO TELEPl10NE MONTil FEBRUARY DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL Olwe Net) i M w e.Neil i | ||
I 553 553 37 1 | |||
2 | 345 553 2 | ||
ig 3 | |||
-5 497 in 221 4 | |||
20 547 5 | |||
379 2 | |||
2.s | 549 484 6 | ||
27 | 22 550 23 217 7 | ||
12 | RTt 8 | ||
538 400 2.s 9 | |||
14 | 541 25 494 10 540 545 26 11 546 27 549 12 516 d | ||
} | -28 551 13 553 | ||
,9, | |||
INSTR UCTIONS | 14 553 30 | ||
On this format.hst the average daily umt power Icelin MWe Net for each day m the reporting month.(ompute to the nearest whole megawatt. | } | ||
15 ERO 3 | |||
16 553 4 | |||
INSTR UCTIONS On this format.hst the average daily umt power Icelin MWe Net for each day m the reporting month.(ompute to the nearest whole megawatt. | |||
tul77 ) | tul77 ) | ||
4 r | 4 r | ||
-w | |||
.. -. -. ~.. - | |||
l UNIT SilUTDOWNS AND POWER REDUCTIONS | l UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO. | ||
50-263 UNIT NAME Mnrit i rel in DATE 1/1/7R COMPLETED BY A-W rabo REPORTMONTis February TELEPHONE 612/295-5151 1 u, | |||
_5 | |||
= | |||
c. | |||
E- | |||
1 | ,E4 Ln.ensee g, | ||
s% | |||
Cause & Cusressive | |||
~,-!e g | |||
4 ise Event s2 s.E Action to L. | |||
Date i | |||
$5 5 | |||
j5g Report : | |||
A0 j' | |||
Presen: Recurrent'e 6 | |||
1 770202 F | |||
31.4 A | |||
1 78-02-01-T SA VALVEX Rod sequence exchange and repair / | |||
inspection of torus vacuum breaker (stuck open).. All torus vacuta breakers tested and adjusted. | inspection of torus vacuum breaker (stuck open).. All torus vacuta breakers tested and adjusted. | ||
2 | 2 770223 F | ||
10.3 | |||
-A-3 N/A IIF ZZZZZE Reactor scram on low condenser vacuum caused by both circulating water pumps tripping from spurious flood protection system signal. | |||
Flood protection system deactivated for further testing. | Flood protection system deactivated for further testing. | ||
1 | 1 2 | ||
1 | 1 4 | ||
C. Refueling | i' Fueced Reaom: | ||
4 Aufum iic S, ram. | \\tethod : | ||
Exhibis G - Insieuiti ms S Sched ufes! | |||
A l~quipment FailureIExplaml | |||
! \\tanual for Prep.iratum of Dara B. Maintenance of Test 2-Manual Scram. | |||
Entry Sheets fe: Ixemcc C. Refueling LOther i E splaml 01616 4 Aufum iic S, ram. | |||
Esent Repori LI RI File INURE G-D-Regulatos) Restiiction. | |||
' t 1 Operator Training & Litenw 1%aminaiam F4dnunistrati.c - | |||
5 G-Operational Es roe ILsplaml Estubit I - Same Source | |||
' p8!77) | |||
Il-Other t (Nplain t i | |||
,=}} | |||
Latest revision as of 14:32, 12 December 2024
| ML20128C616 | |
| Person / Time | |
|---|---|
| Site: | Monticello |
| Issue date: | 02/28/1978 |
| From: | Mayer L, Myrabo A NORTHERN STATES POWER CO. |
| To: | NRC OFFICE OF ADMINISTRATION (ADM) |
| References | |
| NUDOCS 9212040488 | |
| Download: ML20128C616 (5) | |
Text
-
fpA
~
N9N.A,lw,i ucca,_t F..,0PY.
2 NORTHERN 5TATES POWER COMPANY MIN N E A PO LI S. M S N N E GOTA 95404 lkl n..
A
/ ' 'I
'f ') v March 7, 1978
< /d [.
a wa 4 v.s m1973 Q Director, Office of Management O
Information & Program Control C3 c/o Distribution Services Branch, DDC, ADM b
U S Nuclear Regulatory Commission Washington, DC 20555
Dear Sir:
MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 Monthly Operating Report February 1978 Attached are two copies of the Monthly Operating Report for February, 1978 for the Monticello Nuclear Generating Plant.
Yours very truly,
%. U er$
A L 0 Mayer, PE Manager of Nuclear Support Services IDM/ak cc: Director, IE-III, USNRC (1)
(Director, IE, USNRC (c/o DSB) (10)
MPCA Attn: J W Ferman 0
s, t
l 9212040488 780228 780720022 PDR ADOCK 05000263 R
pyg
NARRATIVE SIM4\\Rf 0F OPERATING EXPERIENCE DOCKET NO.
50-263 LNIT 1
l DATE 3/6/78 00$PLETED BY A. L. Mvrabo TELEPIKNE 612/295-5151, Ext. 239
?DNTI Febmary 4
2/1/78 to Operated at 100% of rated power.
2/2/78 2/3/78 Orderly shutdown for rod sequence exchange and re-pair / inspection of tonis vacuum breakers. Trued up bearing housings and bearings and adjusted end clear-ance on toms to drywell vacuum breakers "B" and
" T". Changed out topworks on "A" relief valve due to leak around strainer plug.
2/4/78 Operated at approximately 100% of rated power, except to for weekend reductions to perform control rod exercising 2/22/78 and valve testing.
2/23/78 Reactor scram due to low condenser vacuum caused by both circulating water pumps tripping from spurious flood protection circuit signal.
2/24/78 to Operated at 100% of rated power.
2/28/78 Spent Fuel Storage Update Fuel assemblies in the core - 484 Fuel assemblies in the spent fuel storage pool - 616 Licensed spent fuel storage pool capacity - 740 Date of last refueling that can be discharged with present capacity -Oct, 1978
1 4
1 l
]
OPER ATING DATA REPORT i
DOCKETNO. 50-263 DATE 3/1/78 COMPLETED BY. A.MYRA110 i
TELEPHONE 612/20s.E151 4
.I i
OPERATING STATUS b
Monticello Notes
- 1. Unit Name:
l
- 2. deportmg Period:
Febmarv
.l. Licenwd Thermal Power (MWI):
1670 569
- 4. Nameplate Rating (Grun Mhel.
j
- 5. Design Electrical Rating (Net MWel:
545.4-564 l
- 6. Masimum Dependable Capacity (Gross MWel:
536 7 Masimum Dependahic Capacity (Net MWe):
- h. If Changes Occur in Capacity Ratine titems Number 3 Through 7) Since Last Report. Gise Reawne (Net MWel:
N/A
- 9. Power Letel To Which Restricted.lf Any/A N
i
- 10. Reasons For Restrictions,If Any.:
i j
This Month Yr..to Date Cumulative 1
672 1.416 5_8,441 1 l
- 11. Hours in Reporting Period l
- 12. Number Of Hours Resetor Was Critical 644.2 1.388.2 46.556 6 1.1. Reactor Resene Shutdown Hours 0.0 0.0
-940.7
- 14. Hours Generatm On.Line 630.3 1,374.3 45,151.7 0.0 0.0 0.0
)-
- 15. Unit Resene Shutdown lluurs
- 16. Cross Thermal Energy Generated (MWH) 974.500.8 2.207.824.8 75_.862.399.4
}
- 17. Gruss Electrical Energy Generated (MWH).
334.120_. _,..
756.750 23.129.440
- 15. Net Electrical Energy Generated (MWH) 321.696 729'.302 22'.105.676
~
4
- 19. Unit Senice Factor 93.8%
97.1%
77.3%
93.8%
- 97.lf.
I-
- 20. Unit Availabi:ity Facto,
'7.3%
i l
- 21. Unit Capacity Factor IUsing MDC Neti 89.3%
96.1%
70.6%
87 8%
94 4%-
69.4%
. 2.'
Unit Capacity Factor (Using DER Net)-
- 23. Unit Forced Outage Rate 1.6%
-0.7%
7.8%
- 21. Shutdowns Schedukd User Ne.st 6 Monthy(Type Date,and Duration of Each):
Refueline Outane. October 16. 1978. 40 days
- 25. If Shut Down At End Of Report Period, Estimated Date of Startup:
N/A
- 26. Units in Test Status (Prior to Commercial Operations N/A Forecast
~ Achieved INITI AL CRITICALITY r
INITIA L ELECTRICITY COMMERCI A L OPER ATION
+
i P857 )
1 9'
m A_-,
..A-,
...,m
~m....
..__,a=.,..
~
AVER 4CE D ALLY UNIT POWER LEVEL 50-263 DOCKET NO.
i hbnticello 3,IT DATE 3/1/78 COMPLETED fiY A. hhRABO TELEPl10NE MONTil FEBRUARY DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL Olwe Net) i M w e.Neil i
I 553 553 37 1
345 553 2
ig 3
-5 497 in 221 4
20 547 5
379 2
549 484 6
22 550 23 217 7
RTt 8
538 400 2.s 9
541 25 494 10 540 545 26 11 546 27 549 12 516 d
-28 551 13 553
,9,
14 553 30
}
15 ERO 3
16 553 4
INSTR UCTIONS On this format.hst the average daily umt power Icelin MWe Net for each day m the reporting month.(ompute to the nearest whole megawatt.
tul77 )
4 r
-w
.. -. -. ~.. -
l UNIT SilUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-263 UNIT NAME Mnrit i rel in DATE 1/1/7R COMPLETED BY A-W rabo REPORTMONTis February TELEPHONE 612/295-5151 1 u,
_5
=
c.
E-
,E4 Ln.ensee g,
s%
Cause & Cusressive
~,-!e g
4 ise Event s2 s.E Action to L.
Date i
$5 5
j5g Report :
A0 j'
Presen: Recurrent'e 6
1 770202 F
31.4 A
1 78-02-01-T SA VALVEX Rod sequence exchange and repair /
inspection of torus vacuum breaker (stuck open).. All torus vacuta breakers tested and adjusted.
2 770223 F
10.3
-A-3 N/A IIF ZZZZZE Reactor scram on low condenser vacuum caused by both circulating water pumps tripping from spurious flood protection system signal.
Flood protection system deactivated for further testing.
1 2
1 4
i' Fueced Reaom:
\\tethod :
Exhibis G - Insieuiti ms S Sched ufes!
A l~quipment FailureIExplaml
! \\tanual for Prep.iratum of Dara B. Maintenance of Test 2-Manual Scram.
Entry Sheets fe: Ixemcc C. Refueling LOther i E splaml 01616 4 Aufum iic S, ram.
Esent Repori LI RI File INURE G-D-Regulatos) Restiiction.
' t 1 Operator Training & Litenw 1%aminaiam F4dnunistrati.c -
5 G-Operational Es roe ILsplaml Estubit I - Same Source
' p8!77)
Il-Other t (Nplain t i
,=