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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                            NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                                REGION III
REGION III  
                                    2443 WARRENVILLE RD. SUITE 210
2443 WARRENVILLE RD. SUITE 210  
                                          LISLE, IL 60532-4352
LISLE, IL 60532-4352  
                                        February 10, 2015
Mr. Larry Weber
February 10, 2015  
Senior VP and Chief Nuclear Officer
Indiana Michigan Power Company
Mr. Larry Weber  
Nuclear Generation Group
Senior VP and Chief Nuclear Officer  
One Cook Place
Indiana Michigan Power Company  
Bridgman, MI 49106
Nuclear Generation Group  
SUBJECT: DONALD C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2
One Cook Place  
              NRC INTEGRATED INSPECTION REPORT 05000315/2014005;
Bridgman, MI 49106  
              05000316/2014005
Dear Mr. Weber:
SUBJECT: DONALD C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2  
On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an
NRC INTEGRATED INSPECTION REPORT 05000315/2014005;  
inspection at your Donald C. Cook Nuclear Power Plant, Units 1 and 2. The enclosed report
05000316/2014005  
documents the results of this inspection, which were discussed on January 20, 2015, with
yourself and members of your staff.
Dear Mr. Weber:  
Based on the results of this inspection, three NRC-identified and two self-revealed findings of
On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an  
very low safety significance were identified. The findings involved violations of NRC
inspection at your Donald C. Cook Nuclear Power Plant, Units 1 and 2. The enclosed report  
requirements. However, because of their very low safety significance, and because the issues
documents the results of this inspection, which were discussed on January 20, 2015, with  
were entered into your corrective action program, the NRC is treating the issues as
yourself and members of your staff.  
non-cited violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy
Based on the results of this inspection, three NRC-identified and two self-revealed findings of  
If you contest the subject or severity of these NCVs, you should provide a response within
very low safety significance were identified. The findings involved violations of NRC  
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
requirements. However, because of their very low safety significance, and because the issues  
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a
were entered into your corrective action program, the NRC is treating the issues as
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
non-cited violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy  
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
If you contest the subject or severity of these NCVs, you should provide a response within  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
Office at the Donald C. Cook Nuclear Power Plant. In addition, if you disagree with the
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a  
cross-cutting aspect assigned to any finding in this report, you should provide a response within
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,  
30 days of the date of this inspection report, with the basis for your disagreement, to the
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,  
Regional Administrator, Region III, and the NRC Resident Inspector at the Donald C. Cook
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector  
Office at the Donald C. Cook Nuclear Power Plant. In addition, if you disagree with the  
cross-cutting aspect assigned to any finding in this report, you should provide a response within  
30 days of the date of this inspection report, with the basis for your disagreement, to the  
Regional Administrator, Region III, and the NRC Resident Inspector at the Donald C. Cook  
Nuclear Power Plant.
Nuclear Power Plant.


L. Weber                                       -2-
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy
L. Weber  
of this letter, its enclosure, and your response (if any) will be available electronically for public
-2-  
inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)
component of the NRC's Agencywide Documents Access and Management System (ADAMS).
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public  
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy  
(the Public Electronic Reading Room).
of this letter, its enclosure, and your response (if any) will be available electronically for public  
                                              Sincerely,
inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)  
                                              /RA/
component of the NRC's Agencywide Documents Access and Management System (ADAMS).
                                              Kenneth Riemer, Chief
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html  
                                              Branch 2
(the Public Electronic Reading Room).  
                                              Division of Reactor Projects
Sincerely,  
Docket Nos. 50-315; 50-316
License Nos. DPR-58; DPR-74
/RA/  
Enclosure:
IR 05000315/2014005; 05000316/2014005
  w/Attachment: Supplemental Information
Kenneth Riemer, Chief  
cc w/encl: Distribution via LISTSERV
Branch 2  
Division of Reactor Projects  
Docket Nos. 50-315; 50-316  
License Nos. DPR-58; DPR-74  
Enclosure:  
IR 05000315/2014005; 05000316/2014005  
w/Attachment: Supplemental Information  
cc w/encl: Distribution via LISTSERV  


          U.S. NUCLEAR REGULATORY COMMISSION
                          REGION III
Enclosure
Docket Nos:         05000315; 05000316
U.S. NUCLEAR REGULATORY COMMISSION  
License Nos:       DPR-58; DPR-74
REGION III  
Report No:         05000315/2014005; 05000316/2014005
Docket Nos:  
Licensee:           Indiana Michigan Power Company
05000315; 05000316  
Facility:           Donald C. Cook Nuclear Power Plant, Units 1 and 2
License Nos:  
Location:           Bridgman, MI
DPR-58; DPR-74  
Dates:             October 1 through December 31, 2014
Report No:  
Inspectors:         J. Ellegood, Senior Resident Inspector
05000315/2014005; 05000316/2014005  
                    T. Taylor, Resident Inspector
Licensee:  
                    J. Cassidy, Senior Health Physicist
Indiana Michigan Power Company  
                    M. Garza, Emergency Response Specialist
Facility:  
                    T. Go, Health Physicist
Donald C. Cook Nuclear Power Plant, Units 1 and 2  
                    J. Lennartz, Project Engineer
Location:  
                    M. Mitchell, Health Physicist
Bridgman, MI  
                    M. Phalen, Senior Health Physicist
Dates:  
                    E. Sanchez Santiago, Reactor Inspector
October 1 through December 31, 2014  
Approved by:       Kenneth Riemer, Chief
Inspectors:  
                    Branch 2
J. Ellegood, Senior Resident Inspector  
                    Division of Reactor Projects
                                                                  Enclosure
T. Taylor, Resident Inspector  
J. Cassidy, Senior Health Physicist  
M. Garza, Emergency Response Specialist  
T. Go, Health Physicist
J. Lennartz, Project Engineer
M. Mitchell, Health Physicist  
M. Phalen, Senior Health Physicist  
E. Sanchez Santiago, Reactor Inspector  
Approved by:  
Kenneth Riemer, Chief  
Branch 2  
Division of Reactor Projects  


                                        TABLE OF CONTENTS
SUMMARY OF FINDINGS ........................................................................................................... 2
REPORT DETAILS ....................................................................................................................... 6
TABLE OF CONTENTS  
Summary of Plant Status ........................................................................................................... 6
SUMMARY OF FINDINGS ........................................................................................................... 2  
  1.     REACTOR SAFETY ................................................................................................. 6
REPORT DETAILS ....................................................................................................................... 6  
      1R01   Adverse Weather Protection (71111.01) ............................................................ 6
Summary of Plant Status ........................................................................................................... 6  
      1R04   Equipment Alignment (71111.04) ....................................................................... 7
1.  
      1R05   Fire Protection (71111.05) .................................................................................. 8
REACTOR SAFETY ................................................................................................. 6  
      1R06   Flooding (71111.06) ........................................................................................... 9
1R01  
      1R07   Annual Heat Sink Performance (71111.07) ...................................................... 10
Adverse Weather Protection (71111.01) ............................................................ 6  
      1R08   Inservice Inspection Activities (71111.08P) ...................................................... 10
1R04  
      1R11   Licensed Operator Requalification Program (71111.11) .................................. 13
Equipment Alignment (71111.04) ....................................................................... 7  
      1R12   Maintenance Effectiveness (71111.12) ............................................................ 15
1R05  
      1R13   Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 15
Fire Protection (71111.05) .................................................................................. 8  
      1R15   Operability Determinations and Functional Assessments (71111.15) .............. 16
1R06  
      1R18   Plant Modifications (71111.18) ......................................................................... 21
Flooding (71111.06) ........................................................................................... 9  
      1R19   Post-Maintenance Testing (71111.19) ............................................................. 24
1R07  
      1R20   Outage Activities (71111.20) ............................................................................ 27
Annual Heat Sink Performance (71111.07) ...................................................... 10  
      1R22   Surveillance Testing (71111.22) ....................................................................... 28
1R08  
      1EP4   Emergency Action Level and Emergency Plan Changes (71114.04) ............... 29
Inservice Inspection Activities (71111.08P) ...................................................... 10  
  2.     RADIATION SAFETY ............................................................................................. 31
1R11  
      2RS1   Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 31
Licensed Operator Requalification Program (71111.11) .................................. 13  
      2RS2   Occupational As-Low-As-Reasonably-Achievable Planning and Controls
1R12  
            (71124.02) ........................................................................................................ 37
Maintenance Effectiveness (71111.12) ............................................................ 15  
      2RS7   Radiological Environmental Monitoring Program (71124.07) ........................... 38
1R13
  4.     OTHER ACTIVITIES .............................................................................................. 40
Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 15  
      4OA1   Performance Indicator Verification (71151) ...................................................... 40
1R15  
      4OA2   Identification and Resolution of Problems (71152) ........................................... 45
Operability Determinations and Functional Assessments (71111.15) .............. 16  
      4OA3   Followup of Events and Notices of Enforcement Discretion (71153) ............... 49
1R18  
      4OA6   Management Meetings ..................................................................................... 50
Plant Modifications (71111.18) ......................................................................... 21  
SUPPLEMENTAL INFORMATION ............................................................................................... 1
1R19  
KEY POINTS OF CONTACT..................................................................................................... 1
Post-Maintenance Testing (71111.19) ............................................................. 24  
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 2
1R20  
LIST OF DOCUMENTS REVIEWED......................................................................................... 3
Outage Activities (71111.20) ............................................................................ 27  
LIST OF ACRONYMS USED .................................................................................................. 13
1R22  
Surveillance Testing (71111.22) ....................................................................... 28  
1EP4  
Emergency Action Level and Emergency Plan Changes (71114.04) ............... 29  
2.  
RADIATION SAFETY ............................................................................................. 31  
2RS1  
Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 31  
2RS2  
Occupational As-Low-As-Reasonably-Achievable Planning and Controls  
(71124.02) ........................................................................................................ 37  
2RS7  
Radiological Environmental Monitoring Program (71124.07) ........................... 38  
4.  
OTHER ACTIVITIES .............................................................................................. 40  
4OA1  
Performance Indicator Verification (71151) ...................................................... 40  
4OA2  
Identification and Resolution of Problems (71152) ........................................... 45  
4OA3
Followup of Events and Notices of Enforcement Discretion (71153) ............... 49  
4OA6  
Management Meetings ..................................................................................... 50  
SUPPLEMENTAL INFORMATION ............................................................................................... 1  
KEY POINTS OF CONTACT..................................................................................................... 1  
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 2  
LIST OF DOCUMENTS REVIEWED ......................................................................................... 3  
LIST OF ACRONYMS USED .................................................................................................. 13  


                                        SUMMARY OF FINDINGS
Inspection Report 05000315/2014005, 05000316/2014005; 10/01/2014 - 12/31/2014;
2
Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional
Assessments; Plant Modifications; Post-Maintenance Testing; Radiological Hazard Assessment
SUMMARY OF FINDINGS  
and Exposure Controls.
Inspection Report 05000315/2014005, 05000316/2014005; 10/01/2014 - 12/31/2014;
This report covers a 3-month period of inspection by resident inspectors and announced
Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional  
baseline inspections by regional inspectors. Three Green findings were identified by the
Assessments; Plant Modifications; Post-Maintenance Testing; Radiological Hazard Assessment  
inspectors. Additionally, there were two Green self-revealed findings. The findings were
and Exposure Controls.  
considered non-cited violations (NCVs) of NRC regulations. The significance of inspection
This report covers a 3-month period of inspection by resident inspectors and announced  
findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and
baseline inspections by regional inspectors. Three Green findings were identified by the  
determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process
inspectors. Additionally, there were two Green self-revealed findings. The findings were  
dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Aspects Within the
considered non-cited violations (NCVs) of NRC regulations. The significance of inspection  
Cross-Cutting Areas effective date December 4, 2014. All violations of NRC requirements are
findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and  
dispositioned in accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRC's
determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process  
program for overseeing the safe operation of commercial nuclear power reactors is described in
dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Aspects Within the  
NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014.
Cross-Cutting Areas effective date December 4, 2014. All violations of NRC requirements are  
        Cornerstone: Mitigating Systems
dispositioned in accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRC's  
    *   Green. A finding of very low safety significance, with an associated non-cited violation of
program for overseeing the safe operation of commercial nuclear power reactors is described in  
        10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the
NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014.  
        inspectors for the licensees failure to promptly identify and correct a condition adverse
Cornerstone: Mitigating Systems  
        to quality (CAQ) associated with Unit 1 Turbine-Driven Auxiliary Feedwater (TDAFW)
*  
        pump turbine bearing oil. Specifically, the licensee failed to identify that water was
Green. A finding of very low safety significance, with an associated non-cited violation of  
        entering the oil system after leakage had been identified directly above one of the
10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the  
        TDAFW pump turbine bearings. On April 7, 2014, a cooling water leak was identified
inspectors for the licensees failure to promptly identify and correct a condition adverse  
        above the outboard turbine bearing. The leak was classified as about 1 drop-per-minute
to quality (CAQ) associated with Unit 1 Turbine-Driven Auxiliary Feedwater (TDAFW)  
        (dpm). On April 11, 2014, the licensee discovered the turbine bearing oil level was
pump turbine bearing oil. Specifically, the licensee failed to identify that water was  
        above the maximum mark on an attached sight glass. Several possible reasons were
entering the oil system after leakage had been identified directly above one of the  
        postulated for the high level (which had been steady in-band for over a year), such as
TDAFW pump turbine bearings. On April 7, 2014, a cooling water leak was identified  
        rising turbine building temperatures and the fact that it was not uncommon for personnel
above the outboard turbine bearing. The leak was classified as about 1 drop-per-minute  
        to do unnecessary oil adds to the machine. Oil was drained out until level returned to
(dpm). On April 11, 2014, the licensee discovered the turbine bearing oil level was  
        the maximum mark. On May 22, 2014, the licensee again noted oil level to be above the
above the maximum mark on an attached sight glass. Several possible reasons were  
        maximum mark. Oil was drained again, and similar reasons provided for the level
postulated for the high level (which had been steady in-band for over a year), such as  
        increase. Further, a statement was made that oil level had been steady for the past
rising turbine building temperatures and the fact that it was not uncommon for personnel  
        month, neglecting the previous high level condition. In parallel, NRC inspectors had
to do unnecessary oil adds to the machine. Oil was drained out until level returned to  
        questioned why level was being maintained at the maximum mark when the operator
the maximum mark. On May 22, 2014, the licensee again noted oil level to be above the  
        logs and a sign stated level should be kept at the minimum mark. On May 23, the
maximum mark. Oil was drained again, and similar reasons provided for the level  
        licensee decided to drain the oil system; 620 ml of water was found. New oil was added,
increase. Further, a statement was made that oil level had been steady for the past  
        and a temporary modification was installed which directed leakage away from the
month, neglecting the previous high level condition. In parallel, NRC inspectors had  
        bearing. The issue was entered into the Corrective Action Program (CAP), and an
questioned why level was being maintained at the maximum mark when the operator  
        apparent cause evaluation later determined the leakage to be the primary intrusion
logs and a sign stated level should be kept at the minimum mark. On May 23, the  
        pathway for the water.
licensee decided to drain the oil system; 620 ml of water was found. New oil was added,  
        The issue was more-than-minor because it adversely affected the Configuration Control
and a temporary modification was installed which directed leakage away from the  
        attribute of the Mitigating Systems Cornerstone, whose objective is to ensure the
bearing. The issue was entered into the Corrective Action Program (CAP), and an  
        availability, reliability, and capability of systems that respond to initiating events to
apparent cause evaluation later determined the leakage to be the primary intrusion  
        prevent undesirable consequences. Additionally, if left uncorrected, the issue could lead
pathway for the water.  
        to a more significant safety concern. The inspectors assessed the finding for
The issue was more-than-minor because it adversely affected the Configuration Control  
                                                      2
attribute of the Mitigating Systems Cornerstone, whose objective is to ensure the  
availability, reliability, and capability of systems that respond to initiating events to  
prevent undesirable consequences. Additionally, if left uncorrected, the issue could lead  
to a more significant safety concern. The inspectors assessed the finding for  


  significance using IMC 0609, Significance Determination Process. Per Appendix A, the
  finding screened as Green, or very low safety significance, in Exhibit 2. Specifically, all
3
  questions were answered no under Section A for findings related to Mitigating
  Structures, Systems and Components (SSCs) and Functionality. The inspectors
significance using IMC 0609, Significance Determination Process. Per Appendix A, the  
  reviewed the licensees past operability evaluation and concluded that given the
finding screened as Green, or very low safety significance, in Exhibit 2. Specifically, all  
  projected amount of water that could be entrained in the oil during operation, along with
questions were answered no under Section A for findings related to Mitigating  
  the duration of operation assumed in the safety analyses, that operability of the pump
Structures, Systems and Components (SSCs) and Functionality. The inspectors  
  would be maintained. The finding had an associated cross-cutting aspect in the Human
reviewed the licensees past operability evaluation and concluded that given the  
  Performance area, specifically, H.11, Challenge the Unknown. Regarding the TDAFW
projected amount of water that could be entrained in the oil during operation, along with  
  oil system, the licensee rationalized why the level was increasing without sufficient
the duration of operation assumed in the safety analyses, that operability of the pump  
  investigation given the significance of the system, and did not seek further information
would be maintained. The finding had an associated cross-cutting aspect in the Human  
  that was readily available regarding appropriate oil levels. (Section 1R15)
Performance area, specifically, H.11, Challenge the Unknown. Regarding the TDAFW  
* Green. A finding of very low safety significance, with an associated non-cited violation
oil system, the licensee rationalized why the level was increasing without sufficient  
  of Technical Specification (TS) 5.4, Procedures, was self-revealed when a vacuum was
investigation given the significance of the system, and did not seek further information  
  inadvertently drawn on the AB Fuel Oil Storage Tank (FOST) during preparations for
that was readily available regarding appropriate oil levels. (Section 1R15)  
  surveillance activities. The vacuum caused an indication of lowering level in the tank,
*  
  alarms, and an unplanned TS Limiting Condition for Operation (LCO) action statement
Green. A finding of very low safety significance, with an associated non-cited violation  
  entry. The licensee was performing work activities in preparation for a leak test of the
of Technical Specification (TS) 5.4, Procedures, was self-revealed when a vacuum was  
  FOST. The general sequence of activities should have been a loosening of the vent
inadvertently drawn on the AB Fuel Oil Storage Tank (FOST) during preparations for  
  filter for the tank, a transfer of fuel from the FOST to the Emergency Diesel Generator
surveillance activities. The vacuum caused an indication of lowering level in the tank,  
  (EDG) day tanks, removal of the FOST from service, and finally removal of the vent filter
alarms, and an unplanned TS Limiting Condition for Operation (LCO) action statement  
  so test equipment could be connected to the tank. Due to ambiguous work instruction
entry. The licensee was performing work activities in preparation for a leak test of the  
  steps and activities not being adequately controlled to ensure the proper sequence
FOST. The general sequence of activities should have been a loosening of the vent  
  occurred, workers first removed the vent filter completely and placed a Foreign Material
filter for the tank, a transfer of fuel from the FOST to the Emergency Diesel Generator  
  Exclusion (FME) bag over the vent. When operators later transferred fuel, a vacuum
(EDG) day tanks, removal of the FOST from service, and finally removal of the vent filter  
  was drawn in the tank and level appeared to be going down. Utilizing a manual method
so test equipment could be connected to the tank. Due to ambiguous work instruction  
  of level measurement (which had also been affected by the vacuum), operators
steps and activities not being adequately controlled to ensure the proper sequence  
  determined fuel was actually being lost from the tank to the environment. Shortly
occurred, workers first removed the vent filter completely and placed a Foreign Material  
  thereafter, the bag was found and removed, and level restored to normal (there was no
Exclusion (FME) bag over the vent. When operators later transferred fuel, a vacuum  
  actual loss of fuel). Technical Specification 5.4, Procedures, states, in part, that written
was drawn in the tank and level appeared to be going down. Utilizing a manual method  
  procedures shall be established, implemented, and maintained covering the applicable
of level measurement (which had also been affected by the vacuum), operators  
  procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in
determined fuel was actually being lost from the tank to the environment. Shortly  
  part, that maintenance that can affect the performance of safety-related equipment
thereafter, the bag was found and removed, and level restored to normal (there was no  
  should be properly preplanned and performed in accordance with written procedures,
actual loss of fuel). Technical Specification 5.4, Procedures, states, in part, that written  
  documented instructions, or drawings appropriate to the circumstances. Contrary to
procedures shall be established, implemented, and maintained covering the applicable  
  these requirements, the FOST surveillance was performed with inadequate instructions
procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in  
  and was not coordinated appropriately. The licensee entered the issue into the CAP and
part, that maintenance that can affect the performance of safety-related equipment  
  performed a root cause analysis.
should be properly preplanned and performed in accordance with written procedures,  
  The performance deficiency was more than minor because it adversely impacted the
documented instructions, or drawings appropriate to the circumstances. Contrary to  
  Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is
these requirements, the FOST surveillance was performed with inadequate instructions  
  ensuring the availability, reliability, and capability of systems that respond to initiating
and was not coordinated appropriately. The licensee entered the issue into the CAP and  
  events to prevent undesirable consequences. The finding screened as Green, or very
performed a root cause analysis.  
  low safety significance, utilizing IMC 0609, Appendix A, The Significance Determination
  Process for Findings at Power. Specifically, all questions were answered no under
The performance deficiency was more than minor because it adversely impacted the  
  Section A of Exhibit 2 for Mitigating Systems, since that was the affected cornerstone.
Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is  
  The FME bag was installed, which rendered the AB FOST inoperable, for approximately
ensuring the availability, reliability, and capability of systems that respond to initiating  
  16 hours. This was less than the TS allowed outage time of 48 hours. The finding had
events to prevent undesirable consequences. The finding screened as Green, or very  
  an associated cross-cutting aspect in the human performance area, specifically, H.5,
low safety significance, utilizing IMC 0609, Appendix A, The Significance Determination  
  Work Management. Work activities should be planned, controlled, and executed with
Process for Findings at Power. Specifically, all questions were answered no under  
                                                3
Section A of Exhibit 2 for Mitigating Systems, since that was the affected cornerstone.
The FME bag was installed, which rendered the AB FOST inoperable, for approximately  
16 hours. This was less than the TS allowed outage time of 48 hours. The finding had  
an associated cross-cutting aspect in the human performance area, specifically, H.5,  
Work Management. Work activities should be planned, controlled, and executed with  


  nuclear safety as the overriding priority. Contrary to the tenets of the cross-cutting
  aspect, the work was planned and executed with inadequate work instructions. Further,
4
  there was a lack of coordination between a number of work groups and activities
  associated with the test. (Section 1R15)
nuclear safety as the overriding priority. Contrary to the tenets of the cross-cutting  
* Green. A finding of very low safety significance, with an associated non- violation
aspect, the work was planned and executed with inadequate work instructions. Further,  
  of TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1
there was a lack of coordination between a number of work groups and activities  
  TDAFW pump tripped during an emergent dual-unit shutdown. Both units were taken
associated with the test. (Section 1R15)  
  offline by operators due to debris intrusion from Lake Michigan into the cooling water
  screenhouse. The TDAFW pump started as expected but shutdown after a few minutes
*  
  of operation. Investigation by the licensee revealed that a cover for the trip solenoid had
Green. A finding of very low safety significance, with an associated non- violation
  been installed incorrectly. The cover was relatively loose and had been placed near
of TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1  
  components involved with the proper latching of the Trip and Throttle valve (TTV) (the
TDAFW pump tripped during an emergent dual-unit shutdown. Both units were taken  
  valve which opens to let steam in to turn the pump on). After refuting several possible
offline by operators due to debris intrusion from Lake Michigan into the cooling water  
  causes and running the pump several times for testing, the licensee determined the
screenhouse. The TDAFW pump started as expected but shutdown after a few minutes  
  likely cause of the trip was the misplaced enclosure, which could have interfered with the
of operation. Investigation by the licensee revealed that a cover for the trip solenoid had  
  proper latching of the TTV. Technical Specification 5.4, Procedures, states, in part,
been installed incorrectly. The cover was relatively loose and had been placed near  
  that written procedures shall be established, implemented, and maintained covering the
components involved with the proper latching of the Trip and Throttle valve (TTV) (the  
  applicable procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33
valve which opens to let steam in to turn the pump on). After refuting several possible  
  states, in part, that maintenance that can affect the performance of safety-related
causes and running the pump several times for testing, the licensee determined the  
  equipment should be properly preplanned and performed in accordance with written
likely cause of the trip was the misplaced enclosure, which could have interfered with the  
  procedures, documented instructions, or drawings appropriate to the circumstances.
proper latching of the TTV. Technical Specification 5.4, Procedures, states, in part,  
  Contrary to these requirements, the cause of the misplaced enclosure was due to a lack
that written procedures shall be established, implemented, and maintained covering the  
  of detailed instructions regarding the installation and removal of the enclosure. The
applicable procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33  
  enclosure was most recently affected by maintenance performed during the fall 2014
states, in part, that maintenance that can affect the performance of safety-related  
  refueling outage. The licensee worked with the vendor and reinstalled the enclosure
equipment should be properly preplanned and performed in accordance with written  
  correctly. The Unit 2 TDAFW pump trip solenoid enclosure was also found out of
procedures, documented instructions, or drawings appropriate to the circumstances.
  position and corrected. The licensee entered the issue into the CAP.
Contrary to these requirements, the cause of the misplaced enclosure was due to a lack  
  The performance deficiency was more than minor because it adversely impacted the
of detailed instructions regarding the installation and removal of the enclosure. The  
  Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is
enclosure was most recently affected by maintenance performed during the fall 2014  
  ensuring the availability, reliability, and capability of systems that respond to initiating
refueling outage. The licensee worked with the vendor and reinstalled the enclosure  
  events to prevent undesirable consequences. The inspectors utilized IMC 0609
correctly. The Unit 2 TDAFW pump trip solenoid enclosure was also found out of  
  Appendix A, The Significance Determination Process for Findings at Power, to assess
position and corrected. The licensee entered the issue into the CAP.  
  the significance of the finding. Per Exhibit 2, the finding represented a loss of function
The performance deficiency was more than minor because it adversely impacted the  
  for one train of Auxiliary Feedwater (AFW) for greater than the TS allowed outage time.
Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is  
  Therefore, the inspectors consulted the regional Senior Reactor Analyst for a detailed
ensuring the availability, reliability, and capability of systems that respond to initiating  
  risk evaluation. The inspectors considered the Unit 1 TDAFW pump inoperable since
events to prevent undesirable consequences. The inspectors utilized IMC 0609  
  the last successful surveillance on October 23, 2014. Given the evidence available, this
Appendix A, The Significance Determination Process for Findings at Power, to assess  
  was the likely opportunity for the conditions to be established to set-up the improper
the significance of the finding. Per Exhibit 2, the finding represented a loss of function  
  engagement between the TTV and the trip hook. In the detailed analysis, the finding
for one train of Auxiliary Feedwater (AFW) for greater than the TS allowed outage time.
  screened as Green, or very low safety significance. The finding had an associated
Therefore, the inspectors consulted the regional Senior Reactor Analyst for a detailed  
  cross-cutting aspect in the area of human performance, specifically, H.8, Procedure
risk evaluation. The inspectors considered the Unit 1 TDAFW pump inoperable since  
  Adherence. During maintenance, work proceeded on the trip enclosure despite a lack of
the last successful surveillance on October 23, 2014. Given the evidence available, this  
  detailed instructions on the removal/installation of the enclosure. (Section 1R19)
was the likely opportunity for the conditions to be established to set-up the improper  
  Cornerstone: Barrier Integrity
engagement between the TTV and the trip hook. In the detailed analysis, the finding  
* Green. The inspectors identified a non- violation of 10 CFR Part 50, Appendix B,
screened as Green, or very low safety significance. The finding had an associated  
  Criterion 3 Design Control, for the licensees inadequate radiological review of
cross-cutting aspect in the area of human performance, specifically, H.8, Procedure  
  permanently removing the Auxiliary Missile Blocks (AMBs) from the Unit 1 and Unit 2
Adherence. During maintenance, work proceeded on the trip enclosure despite a lack of  
                                              4
detailed instructions on the removal/installation of the enclosure. (Section 1R19)
Cornerstone: Barrier Integrity  
*  
Green. The inspectors identified a non- violation of 10 CFR Part 50, Appendix B,
Criterion 3 Design Control, for the licensees inadequate radiological review of  
permanently removing the Auxiliary Missile Blocks (AMBs) from the Unit 1 and Unit 2  


  containment accident shields. The finding was determined to be more than minor
  because it was associated with the Barrier Integrity Cornerstone attribute of design
5
  control; and adversely affected the cornerstone objective of maintaining radiological
  barrier functionality of the safety-related accident shield. Specifically, the failure to
containment accident shields. The finding was determined to be more than minor  
  control plant design and adequately evaluate the radiological effects of permanently
because it was associated with the Barrier Integrity Cornerstone attribute of design  
  removing the AMBs from the Unit 1 and Unit 2 containment accident shields did not
control; and adversely affected the cornerstone objective of maintaining radiological  
  ensure that the accident shield will provide its design function to ensure safe radiation
barrier functionality of the safety-related accident shield. Specifically, the failure to  
  levels outside the containment building following a maximum design basis accident.
control plant design and adequately evaluate the radiological effects of permanently  
  The inspectors evaluated the finding using the Significance Determination Process
removing the AMBs from the Unit 1 and Unit 2 containment accident shields did not  
  (SDP) in accordance with IMC 0609, Significance Determination Process, Attachment
ensure that the accident shield will provide its design function to ensure safe radiation  
  0609.04, Initial Characterization of Findings, dated June 19, 2012. Because the finding
levels outside the containment building following a maximum design basis accident.  
  impacted the Barrier Integrity Cornerstone, the inspectors screened the finding through
The inspectors evaluated the finding using the Significance Determination Process  
  IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,
(SDP) in accordance with IMC 0609, Significance Determination Process, Attachment  
  dated June 19, 2012, using Exhibit 3, Barrier Integrity Screening Questions. The
0609.04, Initial Characterization of Findings, dated June 19, 2012. Because the finding  
  finding screened as very-low safety significance (Green) because the finding only
impacted the Barrier Integrity Cornerstone, the inspectors screened the finding through  
  represented a degradation of the radiological barrier function provided for the Auxiliary
IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,  
  Building. The inspectors determined the cause of this finding did not represent current
dated June 19, 2012, using Exhibit 3, Barrier Integrity Screening Questions. The  
  licensee performance and, thus, no cross-cutting aspect was assigned. (Section 1R18)
finding screened as very-low safety significance (Green) because the finding only  
  Cornerstone: Occupational Radiation Safety
represented a degradation of the radiological barrier function provided for the Auxiliary  
* Green. The inspectors identified a finding of very-low safety significance for inadequate
Building. The inspectors determined the cause of this finding did not represent current  
  procedures used to verify Locked High Radiation Controls in the Unit 2 Containment with
licensee performance and, thus, no cross-cutting aspect was assigned. (Section 1R18)  
  an associated non- violation of TS 5.4, Procedures. As a result, weekly, from
Cornerstone: Occupational Radiation Safety  
  November 1, 2013, to March 2014, multiple Radiation Protection Technicians verified the
*  
  Unit 2 Upper Containment Cavity Gate was locked; however it did not secure the area
Green. The inspectors identified a finding of very-low safety significance for inadequate  
  against unauthorized access.
procedures used to verify Locked High Radiation Controls in the Unit 2 Containment with  
  The inspectors determined that the performance deficiency was more than minor
an associated non- violation of TS 5.4, Procedures. As a result, weekly, from  
  because if left uncorrected the performance deficiency could lead to a more significant
November 1, 2013, to March 2014, multiple Radiation Protection Technicians verified the  
  safety concern. Specifically, the failure to identify deficient Locked High Radiation Area
Unit 2 Upper Containment Cavity Gate was locked; however it did not secure the area  
  (LHRA) controls could result in unintentional exposure to high levels of radiation. The
against unauthorized access.  
  finding was determined to be of very-low safety significance because the problem was
The inspectors determined that the performance deficiency was more than minor  
  not an as-low-as-is-reasonably-achievable (ALARA) planning issue, there was no
because if left uncorrected the performance deficiency could lead to a more significant  
  overexposure, nor substantial potential for an overexposure, and the licensees ability to
safety concern. Specifically, the failure to identify deficient Locked High Radiation Area  
  assess dose was not compromised. The inspectors did not identify a corresponding
(LHRA) controls could result in unintentional exposure to high levels of radiation. The  
  cross-cutting aspect for this performance deficiency. The licensee entered the
finding was determined to be of very-low safety significance because the problem was  
  deficiency in their Corrective Action Program as Action Request (AR) 2014-9001
not an as-low-as-is-reasonably-achievable (ALARA) planning issue, there was no  
  immediately upon discovery and presentation by the inspectors. (Section 2RS1.1)
overexposure, nor substantial potential for an overexposure, and the licensees ability to  
                                              5
assess dose was not compromised. The inspectors did not identify a corresponding  
cross-cutting aspect for this performance deficiency. The licensee entered the  
deficiency in their Corrective Action Program as Action Request (AR) 2014-9001  
immediately upon discovery and presentation by the inspectors. (Section 2RS1.1)  


                                        REPORT DETAILS
Summary of Plant Status
6
Unit 1 began the inspection period in a refueling outage. On October 29, 2014, the plant was
restored to 100 percent power. On November 1, rough lake conditions generated substantial
REPORT DETAILS  
amounts of debris that clogged trash racks and travelling screens. The licensee manually
Summary of Plant Status  
tripped the reactor and maintained the plant in hot standby (Mode 3). On November 8, the
Unit 1 began the inspection period in a refueling outage. On October 29, 2014, the plant was  
licensee restored the plant to 100 percent power.
restored to 100 percent power. On November 1, rough lake conditions generated substantial  
Unit 2 began the inspection period at 100 percent power. On November 1, 2014, rough lake
amounts of debris that clogged trash racks and travelling screens. The licensee manually  
conditions generated substantial amounts of debris that clogged trash racks and travelling
tripped the reactor and maintained the plant in hot standby (Mode 3). On November 8, the  
screens. The licensee reduced power to 50 percent to reduce circulating water flow.
licensee restored the plant to 100 percent power.  
Conditions continued to degrade; therefore the licensee manually tripped the reactor. The
Unit 2 began the inspection period at 100 percent power. On November 1, 2014, rough lake  
licensee cooled down and entered Mode 5 to repair an intermediate range nuclear instrument.
conditions generated substantial amounts of debris that clogged trash racks and travelling  
On November 13, the plant was restored to 100 percent power.
screens. The licensee reduced power to 50 percent to reduce circulating water flow.
1.     REACTOR SAFETY
Conditions continued to degrade; therefore the licensee manually tripped the reactor. The  
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
licensee cooled down and entered Mode 5 to repair an intermediate range nuclear instrument.
1R01 Adverse Weather Protection (71111.01)
On November 13, the plant was restored to 100 percent power.
  .1   Winter Seasonal Readiness Preparations
1.  
    a. Inspection Scope
REACTOR SAFETY  
        The inspectors conducted a review of the licensees preparations for winter conditions to
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
        verify that the plants design features and implementation of procedures were sufficient
1R01 Adverse Weather Protection (71111.01)  
        to protect mitigating systems from the effects of adverse weather. Documentation for
.1  
        selected risk-significant systems was reviewed to ensure that these systems would
Winter Seasonal Readiness Preparations  
        remain functional when challenged by inclement weather. During the inspection, the
a.  
        inspectors focused on plant specific design features and the licensees procedures used
Inspection Scope  
        to mitigate or respond to adverse weather conditions. Additionally, the inspectors
The inspectors conducted a review of the licensees preparations for winter conditions to  
        reviewed the Updated Final Safety Analysis Report (UFSAR) and performance
verify that the plants design features and implementation of procedures were sufficient  
        requirements for systems selected for inspection, and verified that operator actions were
to protect mitigating systems from the effects of adverse weather. Documentation for  
        appropriate as specified by plant specific procedures. Cold weather protection, such as
selected risk-significant systems was reviewed to ensure that these systems would  
        heat tracing and area heaters, was verified to be in operation where applicable. The
remain functional when challenged by inclement weather. During the inspection, the  
        inspectors also reviewed CAP items to verify that the licensee was identifying adverse
inspectors focused on plant specific design features and the licensees procedures used  
        weather issues at an appropriate threshold and entering them into their CAP in
to mitigate or respond to adverse weather conditions. Additionally, the inspectors  
        accordance with station corrective action procedures. Documents reviewed are listed in
reviewed the Updated Final Safety Analysis Report (UFSAR) and performance  
        the Attachment to this report. The inspectors reviews focused specifically on the
requirements for systems selected for inspection, and verified that operator actions were  
        following plant systems due to their risk significance or susceptibility to cold weather
appropriate as specified by plant specific procedures. Cold weather protection, such as  
        issues:
heat tracing and area heaters, was verified to be in operation where applicable. The  
        This inspection constituted one winter seasonal readiness preparations sample as
inspectors also reviewed CAP items to verify that the licensee was identifying adverse  
        defined in Inspection Procedure (IP) 71111.01-05.
weather issues at an appropriate threshold and entering them into their CAP in  
    b. Findings
accordance with station corrective action procedures. Documents reviewed are listed in  
        No findings were identified.
the Attachment to this report. The inspectors reviews focused specifically on the  
                                                  6
following plant systems due to their risk significance or susceptibility to cold weather  
issues:  
This inspection constituted one winter seasonal readiness preparations sample as  
defined in Inspection Procedure (IP) 71111.01-05.  
b.  
Findings  
No findings were identified.  


  .2   Readiness for Impending Adverse Weather ConditionHigh Wind Conditions
   
  a. Inspection Scope
7
      On November 6, 2014, the National Weather Service predicted high winds and rough
      lake conditions in the vicinity of the plant. Since debris intrusion during similar conditions
.2  
      the previous week had resulted in damage to equipment and a dual unit plant trip, the
Readiness for Impending Adverse Weather ConditionHigh Wind Conditions
      inspectors validated the sites readiness for the adverse weather. The inspectors
a.  
      reviewed the licensees overall preparations/protection for the expected weather
Inspection Scope  
      conditions. The inspectors walked down the service water screen house to assess the
On November 6, 2014, the National Weather Service predicted high winds and rough  
      licensee progress on repairing trash racks and traveling water screens. The inspectors
lake conditions in the vicinity of the plant. Since debris intrusion during similar conditions  
      evaluated the licensee staffs preparations against the sites procedures and determined
the previous week had resulted in damage to equipment and a dual unit plant trip, the  
      that the staffs actions were adequate. During the inspection, the inspectors focused on
inspectors validated the sites readiness for the adverse weather. The inspectors  
      actions taken to minimize debris intrusion and operators preparations to address
reviewed the licensees overall preparations/protection for the expected weather  
      degradation of raw water systems. The inspectors also reviewed a sample of CAP items
conditions. The inspectors walked down the service water screen house to assess the  
      to verify that the licensee identified adverse weather issues at an appropriate threshold
licensee progress on repairing trash racks and traveling water screens. The inspectors  
      and disposed them through the CAP in accordance with station corrective action
evaluated the licensee staffs preparations against the sites procedures and determined  
      procedures. Documents reviewed are listed in the Attachment to this report.
that the staffs actions were adequate. During the inspection, the inspectors focused on  
      This inspection constituted one readiness for impending adverse weather condition
actions taken to minimize debris intrusion and operators preparations to address  
      sample as defined in IP 71111.01-05.
degradation of raw water systems. The inspectors also reviewed a sample of CAP items  
  b. Findings
to verify that the licensee identified adverse weather issues at an appropriate threshold  
      No findings were identified.
and disposed them through the CAP in accordance with station corrective action  
1R04 Equipment Alignment (71111.04)
procedures. Documents reviewed are listed in the Attachment to this report.  
.1   Quarterly Partial System Walkdowns
This inspection constituted one readiness for impending adverse weather condition  
  a. Inspection Scope
sample as defined in IP 71111.01-05.  
      The inspectors performed partial system walkdowns of the following risk-significant
b.  
      systems:
Findings  
      *       Unit 2 Residual Heat Removal system after maintenance;
No findings were identified.  
      *       Unit 2 Steam Generator (SG) power-operated relief valves during maintenance
1R04 Equipment Alignment (71111.04)  
              on other power-operated relief valves; and
.1  
      *       Unit 2 AFW during maintenance on a single train.
Quarterly Partial System Walkdowns  
      The inspectors selected these systems based on their risk significance relative to the
a.  
      Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
Inspection Scope  
      to identify any discrepancies that could impact the function of the system and, therefore,
The inspectors performed partial system walkdowns of the following risk-significant  
      potentially increase risk. The inspectors reviewed applicable operating procedures,
systems:  
      system diagrams, UFSAR, TS requirements, outstanding work orders (WOs), condition
*  
      reports, and the impact of ongoing work activities on redundant trains of equipment in
Unit 2 Residual Heat Removal system after maintenance;  
      order to identify conditions that could have rendered the systems incapable of
*  
      performing their intended functions. The inspectors also walked down accessible
Unit 2 Steam Generator (SG) power-operated relief valves during maintenance  
      portions of the systems to verify system components and support equipment were
on other power-operated relief valves; and  
      aligned correctly and operable. The inspectors examined the material condition of the
*  
      components and observed operating parameters of equipment to verify that there were
Unit 2 AFW during maintenance on a single train.  
      no obvious deficiencies. The inspectors also verified that the licensee had properly
The inspectors selected these systems based on their risk significance relative to the  
                                                  7
Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted  
to identify any discrepancies that could impact the function of the system and, therefore,  
potentially increase risk. The inspectors reviewed applicable operating procedures,  
system diagrams, UFSAR, TS requirements, outstanding work orders (WOs), condition  
reports, and the impact of ongoing work activities on redundant trains of equipment in  
order to identify conditions that could have rendered the systems incapable of  
performing their intended functions. The inspectors also walked down accessible  
portions of the systems to verify system components and support equipment were  
aligned correctly and operable. The inspectors examined the material condition of the  
components and observed operating parameters of equipment to verify that there were  
no obvious deficiencies. The inspectors also verified that the licensee had properly  


      identified and resolved equipment alignment problems that could cause initiating events
      or impact the capability of mitigating systems or barriers and entered them into the CAP
8
      with the appropriate significance characterization. Documents reviewed are listed in the
      Attachment to this report.
identified and resolved equipment alignment problems that could cause initiating events  
      These activities constituted three partial system walkdown samples as defined in
or impact the capability of mitigating systems or barriers and entered them into the CAP  
      IP 71111.04-05.
with the appropriate significance characterization. Documents reviewed are listed in the  
  b. Findings
Attachment to this report.  
      No findings were identified.
These activities constituted three partial system walkdown samples as defined in  
.2   Semiannual Complete System Walkdown
IP 71111.04-05.  
  a. Inspection Scope
b.  
      On December 30, 2014, the inspectors completed a complete system alignment
Findings  
      inspection of the Unit 1 Containment Spray system to verify the functional capability of
No findings were identified.  
      the system. This system was selected because it was considered both safety significant
.2  
      and risk significant in the licensees probabilistic risk assessment. The inspectors
Semiannual Complete System Walkdown  
      walked down the system to review mechanical and electrical equipment lineups;
a.  
      electrical power availability; system pressure and temperature indications, as
Inspection Scope  
      appropriate; component labeling; component lubrication; component and equipment
On December 30, 2014, the inspectors completed a complete system alignment  
      cooling; hangers and supports; operability of support systems; and to ensure that
inspection of the Unit 1 Containment Spray system to verify the functional capability of  
      ancillary equipment or debris did not interfere with equipment operation. A review of a
the system. This system was selected because it was considered both safety significant  
      sample of past and outstanding WOs was performed to determine whether any
and risk significant in the licensees probabilistic risk assessment. The inspectors  
      deficiencies significantly affected the system function. In addition, the inspectors
walked down the system to review mechanical and electrical equipment lineups;  
      reviewed the CAP database to ensure that system equipment alignment problems were
electrical power availability; system pressure and temperature indications, as  
      being identified and appropriately resolved. Documents reviewed are listed in the
appropriate; component labeling; component lubrication; component and equipment  
      Attachment to this report.
cooling; hangers and supports; operability of support systems; and to ensure that  
      These activities constituted one complete system walkdown sample as defined in
ancillary equipment or debris did not interfere with equipment operation. A review of a  
      IP 71111.04-05.
sample of past and outstanding WOs was performed to determine whether any  
  b. Findings
deficiencies significantly affected the system function. In addition, the inspectors  
      No findings were identified.
reviewed the CAP database to ensure that system equipment alignment problems were  
1R05 Fire Protection (71111.05)
being identified and appropriately resolved. Documents reviewed are listed in the  
.1   Routine Resident Inspector Tours (71111.05Q)
Attachment to this report.  
  a. Inspection Scope
These activities constituted one complete system walkdown sample as defined in  
      The inspectors conducted fire protection walkdowns which were focused on availability,
IP 71111.04-05.  
      accessibility, and the condition of firefighting equipment in the following risk-significant
b.  
      plant areas:
Findings  
      *       Unit 2 AB EDG;
No findings were identified.  
      *       Unit 2 CD EDG;
1R05 Fire Protection (71111.05)  
      *       Unit 2 Quadrant cable tunnels; and
.1  
      *       Unit 1 Essential Service Water Motor Control Center Room.
Routine Resident Inspector Tours (71111.05Q)  
                                                  8
a.  
Inspection Scope  
The inspectors conducted fire protection walkdowns which were focused on availability,  
accessibility, and the condition of firefighting equipment in the following risk-significant  
plant areas:  
*  
Unit 2 AB EDG;  
*  
Unit 2 CD EDG;  
*  
Unit 2 Quadrant cable tunnels; and  
*  
Unit 1 Essential Service Water Motor Control Center Room.  


      The inspectors reviewed areas to assess if the licensee had implemented a fire
      protection program that adequately controlled combustibles and ignition sources
9
      within the plant, effectively maintained fire detection and suppression capability,
      maintained passive fire protection features in good material condition, and implemented
The inspectors reviewed areas to assess if the licensee had implemented a fire  
      adequate compensatory measures for out-of-service, degraded or inoperable fire
protection program that adequately controlled combustibles and ignition sources  
      protection equipment, systems, or features in accordance with the licensees fire plan.
within the plant, effectively maintained fire detection and suppression capability,  
      The inspectors selected fire areas based on their overall contribution to internal fire risk
maintained passive fire protection features in good material condition, and implemented  
      as documented in the plants Individual Plant Examination of External Events with later
adequate compensatory measures for out-of-service, degraded or inoperable fire  
      additional insights, their potential to impact equipment which could initiate or mitigate a
protection equipment, systems, or features in accordance with the licensees fire plan.
      plant transient, or their impact on the plants ability to respond to a security event.
The inspectors selected fire areas based on their overall contribution to internal fire risk  
      Using the documents listed in the Attachment to this report, the inspectors verified that
as documented in the plants Individual Plant Examination of External Events with later  
      fire hoses and extinguishers were in their designated locations and available for
additional insights, their potential to impact equipment which could initiate or mitigate a  
      immediate use; that fire detectors and sprinklers were unobstructed; that transient
plant transient, or their impact on the plants ability to respond to a security event.
      material loading was within the analyzed limits; and fire doors, dampers, and penetration
Using the documents listed in the Attachment to this report, the inspectors verified that  
      seals appeared to be in satisfactory condition. The inspectors also verified that minor
fire hoses and extinguishers were in their designated locations and available for  
      issues identified during the inspection were entered into the licensees CAP.
immediate use; that fire detectors and sprinklers were unobstructed; that transient  
      Documents reviewed are listed in the Attachment to this report.
material loading was within the analyzed limits; and fire doors, dampers, and penetration  
      These activities constituted four quarterly fire protection inspection samples as defined in
seals appeared to be in satisfactory condition. The inspectors also verified that minor  
      IP 71111.05-05.
issues identified during the inspection were entered into the licensees CAP.
  b. Findings
Documents reviewed are listed in the Attachment to this report.  
      No findings were identified.
These activities constituted four quarterly fire protection inspection samples as defined in  
1R06 Flooding (71111.06)
IP 71111.05-05.  
.1   Underground Vaults
b.  
  a. Inspection Scope
Findings  
      The inspectors selected underground bunkers/manholes subject to flooding that
No findings were identified.  
      contained cables whose failure could disable risk-significant equipment. The inspectors
1R06 Flooding (71111.06)  
      determined that the cables were not submerged, that splices were intact, and that
.1  
      appropriate cable support structures were in place. In those areas where dewatering
Underground Vaults  
      devices were used, such as a sump pump, the device was operable and level alarm
a.  
      circuits were set appropriately to ensure that the cables would not be submerged. In
Inspection Scope  
      those areas without dewatering devices, the inspectors verified that drainage of the area
The inspectors selected underground bunkers/manholes subject to flooding that  
      was available, or that the cables were qualified for submergence conditions. The
contained cables whose failure could disable risk-significant equipment. The inspectors  
      inspectors also reviewed the licensees corrective action documents with respect to past
determined that the cables were not submerged, that splices were intact, and that  
      submerged cable issues identified in the corrective action program to verify the
appropriate cable support structures were in place. In those areas where dewatering  
      adequacy of the corrective actions. The inspectors performed a walkdown of the
devices were used, such as a sump pump, the device was operable and level alarm  
      following underground bunkers/manholes subject to flooding:
circuits were set appropriately to ensure that the cables would not be submerged. In  
      *       Bunkers/manholes containing security cabling; and
those areas without dewatering devices, the inspectors verified that drainage of the area  
      *       Bunkers/manholes with safety-related cabling supporting technical specification
was available, or that the cables were qualified for submergence conditions. The  
              offsite power sources
inspectors also reviewed the licensees corrective action documents with respect to past  
      Specific documents reviewed during this inspection are listed in the Attachment to this
submerged cable issues identified in the corrective action program to verify the  
      report. This inspection constituted one underground vaults sample as defined in
adequacy of the corrective actions. The inspectors performed a walkdown of the  
      IP 71111.06-05.
following underground bunkers/manholes subject to flooding:  
                                                9
*  
Bunkers/manholes containing security cabling; and  
*  
Bunkers/manholes with safety-related cabling supporting technical specification  
offsite power sources  
Specific documents reviewed during this inspection are listed in the Attachment to this  
report. This inspection constituted one underground vaults sample as defined in  
IP 71111.06-05.  


  b. Findings
      No findings were identified.
10
1R07 Annual Heat Sink Performance (71111.07)
  a. Inspection Scope
b.  
      The inspectors reviewed the licensees inspection of Unit 1 CD EDG north air aftercooler
Findings  
      to verify that potential deficiencies did not mask the licensees ability to detect degraded
No findings were identified.  
      performance, to identify any common cause issues that had the potential to increase
1R07 Annual Heat Sink Performance (71111.07)  
      risk, and to ensure that the licensee was adequately addressing problems that could
a.  
      result in initiating events that would cause an increase in risk. The inspectors observed
Inspection Scope  
      licensee visual observations of the internals of the heat exchanger to verify cleanliness
The inspectors reviewed the licensees inspection of Unit 1 CD EDG north air aftercooler  
      of the heat exchanger. Additionally, the inspectors reviewed eddy current testing results
to verify that potential deficiencies did not mask the licensees ability to detect degraded  
      and interviewed heat exchanger program engineers. Documents reviewed for this
performance, to identify any common cause issues that had the potential to increase  
      inspection are listed in the Attachment to this document.
risk, and to ensure that the licensee was adequately addressing problems that could  
      This annual heat sink performance inspection constituted one sample as defined in
result in initiating events that would cause an increase in risk. The inspectors observed  
      IP 71111.07-05.
licensee visual observations of the internals of the heat exchanger to verify cleanliness  
  b. Findings
of the heat exchanger. Additionally, the inspectors reviewed eddy current testing results  
      No findings were identified.
and interviewed heat exchanger program engineers. Documents reviewed for this  
1R08 Inservice Inspection Activities (71111.08P)
inspection are listed in the Attachment to this document.  
      From September 29, 2014, through October 10, 2014, the inspector conducted a review
This annual heat sink performance inspection constituted one sample as defined in  
      of the implementation of the licensees Inservice Inspection (ISI) Program for monitoring
IP 71111.07-05.  
      degradation of the Unit 1 Reactor Coolant System (RCS), steam generator tubes,
b.  
      Emergency Feedwater Systems, Risk Significant Piping and Components, and
Findings  
      Containment Systems.
No findings were identified.  
      The inspections described in Sections 1R08.1, 1R08.2, IR08.3, IR08.4, and 1R08.5
1R08 Inservice Inspection Activities (71111.08P)  
      below constituted one inservice inspection sample as defined in IP 71111.08-05.
From September 29, 2014, through October 10, 2014, the inspector conducted a review  
.1   Piping Systems Inservice Inspection
of the implementation of the licensees Inservice Inspection (ISI) Program for monitoring  
  a. Inspection Scope
degradation of the Unit 1 Reactor Coolant System (RCS), steam generator tubes,  
      The inspectors observed and reviewed records of the following non-destructive
Emergency Feedwater Systems, Risk Significant Piping and Components, and  
      examinations (NDE) mandated by the American Society of Mechanical Engineers
Containment Systems.  
      (ASME) Section XI Code to evaluate compliance with the ASME Code Section XI
The inspections described in Sections 1R08.1, 1R08.2, IR08.3, IR08.4, and 1R08.5  
      and Section V requirements, and if any indications and defects were detected, to
below constituted one inservice inspection sample as defined in IP 71111.08-05.  
      determine whether these were dispositioned in accordance with the ASME Code or an
.1  
      NRC-approved alternative requirement:
Piping Systems Inservice Inspection  
      *       Ultrasonic (UT) examination of ASME Code Class 2, risk informed (R-A), pipe to
a.  
              elbow weld, 1-FW-12-02S;
Inspection Scope  
      *       UT of ASME Code Class 1, Pressurizer Relief Nozzle inner Radius;
The inspectors observed and reviewed records of the following non-destructive  
              6-1-RC-7-IRS;
examinations (NDE) mandated by the American Society of Mechanical Engineers  
                                                10
(ASME) Section XI Code to evaluate compliance with the ASME Code Section XI  
and Section V requirements, and if any indications and defects were detected, to  
determine whether these were dispositioned in accordance with the ASME Code or an  
NRC-approved alternative requirement:  
*  
Ultrasonic (UT) examination of ASME Code Class 2, risk informed (R-A), pipe to  
elbow weld, 1-FW-12-02S;  
*  
UT of ASME Code Class 1, Pressurizer Relief Nozzle inner Radius;  
6-1-RC-7-IRS;  


    *       UT of ASME Code Class 1; Pressurizer Spray Nozzle Inner Radius;
            4-1-RC-10-IRS; and
11
    *       Magnetic Particle (MT) Examination of ASME Code Class 1, Pressurizer Vessel
            Support; 1-PRZ-26.
*  
    There were no recordable indications identified during the previous refueling outage.
UT of ASME Code Class 1; Pressurizer Spray Nozzle Inner Radius;  
    The inspectors reviewed NDE records associated with the following pressure boundary
4-1-RC-10-IRS; and  
    welds completed for risk significant components during the current refueling outage to
*  
    determine whether the licensee applied the pre-service NDE and acceptance criteria
Magnetic Particle (MT) Examination of ASME Code Class 1, Pressurizer Vessel  
    required by the Construction Code and ASME Code, Section XI. Additionally, the
Support; 1-PRZ-26.  
    inspectors reviewed the welding procedure specification and supporting weld procedure
There were no recordable indications identified during the previous refueling outage.  
    qualification records to determine whether the weld procedure was qualified in
The inspectors reviewed NDE records associated with the following pressure boundary  
    accordance with the requirements of Construction Code and the ASME Code Section IX:
welds completed for risk significant components during the current refueling outage to  
    *       Welds OW-1, OW-2 and OW-3 associated with replacement valve 1-CS-314
determine whether the licensee applied the pre-service NDE and acceptance criteria  
            (Work Order 55440759-5); and
required by the Construction Code and ASME Code, Section XI. Additionally, the  
    *       Welds OW-1 and OW-2 associated with replacement valve 1-NLI-112-V1 (Work
inspectors reviewed the welding procedure specification and supporting weld procedure  
            Order 55390312-01)
qualification records to determine whether the weld procedure was qualified in  
    The inspectors also reviewed NDE records associated with the following pressure
accordance with the requirements of Construction Code and the ASME Code Section IX:  
    boundary welds completed for risk significant systems since the beginning of the last
*  
    refueling:
Welds OW-1, OW-2 and OW-3 associated with replacement valve 1-CS-314  
    *       Welds OW-1, 2, 3, 4, 5 and OW-6 associated with replacement of valve
(Work Order 55440759-5); and  
            1-NFP-222-V2 (Work Order 55421212-10/13); and
*  
    *       Welds OW-1 associated with the installation of pipe support 1-ARC-S4012
Welds OW-1 and OW-2 associated with replacement valve 1-NLI-112-V1 (Work  
            (WO Order 55404504-06).
Order 55390312-01)  
  b. Findings
The inspectors also reviewed NDE records associated with the following pressure  
    No findings were identified.
boundary welds completed for risk significant systems since the beginning of the last  
.2   Reactor Pressure Vessel Upper Head Penetration Inspection Activities
refueling:  
  a. Inspection Scope
*  
    For the Unit 1 reactor vessel head, no examination was required pursuant to
Welds OW-1, 2, 3, 4, 5 and OW-6 associated with replacement of valve  
    10 CFR 50.55a(g)(6)(ii)(D) for the current refueling outage. Therefore, no NRC review
1-NFP-222-V2 (Work Order 55421212-10/13); and  
    was completed for this inspection procedure attribute.
*  
  b. Findings
Welds OW-1 associated with the installation of pipe support 1-ARC-S4012  
    No findings were identified.
(WO Order 55404504-06).  
.3   Boric Acid Corrosion Control (BACC)
b.  
  a. Inspection Scope
Findings  
    The inspectors observed the licensees BACC visual examinations for portions of the
No findings were identified.  
    RCS, connected systems, and verified whether these visual examinations emphasized
.2  
                                            11
Reactor Pressure Vessel Upper Head Penetration Inspection Activities  
a.  
Inspection Scope  
For the Unit 1 reactor vessel head, no examination was required pursuant to  
10 CFR 50.55a(g)(6)(ii)(D) for the current refueling outage. Therefore, no NRC review  
was completed for this inspection procedure attribute.
b.  
Findings  
No findings were identified.  
.3  
Boric Acid Corrosion Control (BACC)  
a.  
Inspection Scope  
The inspectors observed the licensees BACC visual examinations for portions of the  
RCS, connected systems, and verified whether these visual examinations emphasized  


      locations where boric acid leaks can cause degradation of safety significant
      components.
12
      The inspectors reviewed the following licensee evaluations of RCS components with
      Boric Acid deposits to determine whether degraded components were documented in
locations where boric acid leaks can cause degradation of safety significant  
      the corrective action system. The inspectors also evaluated corrective actions for any
components.  
      degraded RCS components to determine whether they met the component Construction
The inspectors reviewed the following licensee evaluations of RCS components with  
      Code, ASME Section XI Code, and/or NRC approved alternative:
Boric Acid deposits to determine whether degraded components were documented in  
      *       AR 2013-4317; 1-QRV-114, body to bonnet leak;
the corrective action system. The inspectors also evaluated corrective actions for any  
      *       AR 2013-4625;1-CS-448-1 has a BA leak;
degraded RCS components to determine whether they met the component Construction  
      *       AR 2013-5096; No. 14 SG cold leg nozzle dam leakage;
Code, ASME Section XI Code, and/or NRC approved alternative:  
      *       AR 2013-6839; U1C25 Refueling Cavity Leakage; and
*  
      *       AR 2013-7061; 1-RH-147W has Boric Acid on Body to Bonnet.
AR 2013-4317; 1-QRV-114, body to bonnet leak;  
      The inspectors reviewed the following corrective actions related to evidence of
*  
      BA leakage to determine whether the corrective actions completed were consistent with
AR 2013-4625;1-CS-448-1 has a BA leak;  
      the requirements of the ASME Code Section XI and 10 CFR Part 50, Appendix B,
*  
      Criterion XVI:
AR 2013-5096; No. 14 SG cold leg nozzle dam leakage;  
      *       AR 2013-0534; 12-CS-185 has a body to bonnet leak;
*  
      *       AR 2014-9459; 12-CS-185 has a ruptured diaphragm;
AR 2013-6839; U1C25 Refueling Cavity Leakage; and  
      *       AR 2013-7220; Reactor Head and Pressure Vent Piping Area;
*  
      *       AR 2013-7355; 1-NFP-240 has evidence of prior test fitting leakage; and
AR 2013-7061; 1-RH-147W has Boric Acid on Body to Bonnet.  
      *       AR 2013-7067; 1-RH-107W leaks by at 0.095 ml/min.
The inspectors reviewed the following corrective actions related to evidence of  
  b. Findings
BA leakage to determine whether the corrective actions completed were consistent with  
      No findings were identified.
the requirements of the ASME Code Section XI and 10 CFR Part 50, Appendix B,  
.4   Steam Generator Tube Inspection Activities
Criterion XVI:  
  a. Inspection Scope
*  
      The NRC inspectors observed acquisition of eddy current (ET) data, interviewed ET data
AR 2013-0534; 12-CS-185 has a body to bonnet leak;  
      analysts, and reviewed documentation related to the SG ISI Program to determine
*  
      whether:
AR 2014-9459; 12-CS-185 has a ruptured diaphragm;  
      *       the numbers and sizes of SG tube flaws/degradation identified was consistent
*  
              with the licensees previous outage Operational Assessment predictions;
AR 2013-7220; Reactor Head and Pressure Vent Piping Area;  
      *       the SG tube ET examination scope and expansion criteria were sufficient to meet
*  
              the Technical Specifications, and the Electric Power Research Institute (EPRI)
AR 2013-7355; 1-NFP-240 has evidence of prior test fitting leakage; and  
              Document 1013706, Pressurized Water Reactor Steam Generator Examination
*  
              Guidelines;
AR 2013-7067; 1-RH-107W leaks by at 0.095 ml/min.  
      *       the SG tube ET examination scope included potential areas of tube degradation
b. Findings  
              identified in prior outage SG tube inspections and/or as identified in NRC generic
No findings were identified.  
              industry operating experience applicable to these SG tubes;
.4  
      *       the licensee-identified new tube degradation mechanisms and implemented
Steam Generator Tube Inspection Activities  
              adequate extent of condition inspection scope and repairs for the new tube
a.  
              degradation mechanism;
Inspection Scope  
      *       the licensee implemented qualified depth sizing methods to degraded tubes
The NRC inspectors observed acquisition of eddy current (ET) data, interviewed ET data  
              accepted for continued service;
analysts, and reviewed documentation related to the SG ISI Program to determine  
                                              12
whether:  
*  
the numbers and sizes of SG tube flaws/degradation identified was consistent  
with the licensees previous outage Operational Assessment predictions;  
*  
the SG tube ET examination scope and expansion criteria were sufficient to meet  
the Technical Specifications, and the Electric Power Research Institute (EPRI)  
Document 1013706, Pressurized Water Reactor Steam Generator Examination  
Guidelines;  
*  
the SG tube ET examination scope included potential areas of tube degradation  
identified in prior outage SG tube inspections and/or as identified in NRC generic  
industry operating experience applicable to these SG tubes;  
*  
the licensee-identified new tube degradation mechanisms and implemented  
adequate extent of condition inspection scope and repairs for the new tube  
degradation mechanism;  
*  
the licensee implemented qualified depth sizing methods to degraded tubes  
accepted for continued service;  


      *       the ET probes and equipment configurations used to acquire data from the SG
                tubes were qualified to detect the known/expected types of SG tube degradation
13
                in accordance with Appendix H, Performance Demonstration for Eddy Current
                Examination, of EPRI Document 1013706, Pressurized Water Reactor Steam
*  
                Generator Examination Guidelines;
the ET probes and equipment configurations used to acquire data from the SG  
      *       the licensee performed secondary side SG inspections for location and removal
tubes were qualified to detect the known/expected types of SG tube degradation  
                of foreign materials;
in accordance with Appendix H, Performance Demonstration for Eddy Current  
      *       The licensee implemented repairs for SG tubes damaged by foreign material;
Examination, of EPRI Document 1013706, Pressurized Water Reactor Steam  
                and
Generator Examination Guidelines;
      *       Foreign objects were left within the secondary side of the SGs, and if so, that the
*  
                licensee implemented evaluations, which included the effects of foreign object
the licensee performed secondary side SG inspections for location and removal  
                migration and/or tube fretting damage.
of foreign materials;  
  b. Findings
*  
      No findings were identified.
The licensee implemented repairs for SG tubes damaged by foreign material;  
.5   Identification and Resolution of Problems
and  
    a. Inspection Scope
*  
      The inspectors performed a review of ISI-related problems entered into the licensees
Foreign objects were left within the secondary side of the SGs, and if so, that the  
      CAP and conducted interviews with licensee staff to determine whether:
licensee implemented evaluations, which included the effects of foreign object  
      *       the licensee had established an appropriate threshold for identifying ISI-related
migration and/or tube fretting damage.  
                problems;
b.  
      *       the licensee had performed a root cause (if applicable) and taken appropriate
Findings  
                corrective actions; and
No findings were identified.  
      *       the licensee had evaluated operating experience and industry generic issues
.5  
                related to ISI and pressure boundary integrity.
Identification and Resolution of Problems  
      The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,
a. Inspection Scope  
      Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action
The inspectors performed a review of ISI-related problems entered into the licensees  
      documents reviewed by the inspectors are listed in the Attachment to this report.
CAP and conducted interviews with licensee staff to determine whether:  
    b. Findings
*  
      No findings were identified.
the licensee had established an appropriate threshold for identifying ISI-related  
1R11 Licensed Operator Requalification Program (71111.11)
problems;  
.1   Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)
*  
  a. Inspection Scope
the licensee had performed a root cause (if applicable) and taken appropriate  
      On November 19, 2014, the inspectors observed a crew of licensed operators in the
corrective actions; and  
      plants simulator during licensed operator requalification training to verify that operator
*  
      performance was adequate, evaluators were identifying and documenting crew
the licensee had evaluated operating experience and industry generic issues  
      performance problems and training was being conducted in accordance with licensee
related to ISI and pressure boundary integrity.  
      procedures. The inspectors evaluated the following areas:
The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,  
      *       licensed operator performance;
Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action  
                                                  13
documents reviewed by the inspectors are listed in the Attachment to this report.  
b. Findings  
No findings were identified.  
1R11 Licensed Operator Requalification Program (71111.11)  
.1  
Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)  
a.  
Inspection Scope  
On November 19, 2014, the inspectors observed a crew of licensed operators in the  
plants simulator during licensed operator requalification training to verify that operator  
performance was adequate, evaluators were identifying and documenting crew  
performance problems and training was being conducted in accordance with licensee  
procedures. The inspectors evaluated the following areas:  
*  
licensed operator performance;  


    *       crews clarity and formality of communications;
    *       ability to take timely actions in the conservative direction;
14
    *       prioritization, interpretation, and verification of annunciator alarms;
    *       correct use and implementation of abnormal and emergency procedures;
*  
    *       control board manipulations;
crews clarity and formality of communications;  
    *       oversight and direction from supervisors; and
*  
    *       ability to identify and implement appropriate TS actions and Emergency Plan
ability to take timely actions in the conservative direction;  
              actions and notifications.
*  
    The crews performance in these areas was compared to pre-established operator action
prioritization, interpretation, and verification of annunciator alarms;  
    expectations and successful critical task completion requirements. Documents reviewed
*  
    are listed in the Attachment to this report.
correct use and implementation of abnormal and emergency procedures;  
    This inspection constituted one quarterly licensed operator requalification program
*  
    simulator sample as defined in IP 71111.11
control board manipulations;  
  b. Findings
*  
    No findings were identified.
oversight and direction from supervisors; and  
.2   Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)
*  
  a. Inspection Scope
ability to identify and implement appropriate TS actions and Emergency Plan  
    On October 17-18, 2014, the inspectors observed the drain-down and vacuum fill of the
actions and notifications.  
    RCS during the Unit 1 refueling outage. This was a high-risk (Orange) activity planned
The crews performance in these areas was compared to pre-established operator action  
    during the outage. The inspectors evaluated the following areas:
expectations and successful critical task completion requirements. Documents reviewed  
    *       licensed operator performance;
are listed in the Attachment to this report.  
    *       crews clarity and formality of communications;
This inspection constituted one quarterly licensed operator requalification program  
    *       ability to take timely actions in the conservative direction;
simulator sample as defined in IP 71111.11
    *       prioritization, interpretation, and verification of annunciator alarms (if applicable);
b.  
    *       correct use and implementation of procedures;
Findings  
    *       control board (or equipment) manipulations;
No findings were identified.  
    *       oversight and direction from supervisors; and
.2  
    *       ability to identify and implement appropriate TS actions and Emergency Plan
Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)  
              actions and notifications (if applicable).
a.  
    The performance in these areas was compared to pre-established operator action
Inspection Scope  
    expectations, procedural compliance and task completion requirements. Documents
On October 17-18, 2014, the inspectors observed the drain-down and vacuum fill of the  
    reviewed are listed in the Attachment to this report.
RCS during the Unit 1 refueling outage. This was a high-risk (Orange) activity planned  
    This inspection constituted one quarterly licensed operator heightened activity/risk
during the outage. The inspectors evaluated the following areas:  
    sample as defined in IP 71111.11, and was done in conjunction with the requirements of
*  
    IP 71111.20.
licensed operator performance;  
                                                  14
*  
crews clarity and formality of communications;  
*  
ability to take timely actions in the conservative direction;  
*  
prioritization, interpretation, and verification of annunciator alarms (if applicable);  
*  
correct use and implementation of procedures;  
*  
control board (or equipment) manipulations;  
*  
oversight and direction from supervisors; and  
*  
ability to identify and implement appropriate TS actions and Emergency Plan  
actions and notifications (if applicable).  
The performance in these areas was compared to pre-established operator action  
expectations, procedural compliance and task completion requirements. Documents  
reviewed are listed in the Attachment to this report.  
This inspection constituted one quarterly licensed operator heightened activity/risk  
sample as defined in IP 71111.11, and was done in conjunction with the requirements of  
IP 71111.20.  


1R12 Maintenance Effectiveness (71111.12)
  a. Inspection Scope
15
    The inspectors evaluated degraded performance issues involving the following
    risk-significant systems:
1R12 Maintenance Effectiveness (71111.12)  
    *       Nuclear Instrumentation;
a.  
    *       Main Steam;
Inspection Scope  
    *       Anticipated Transient Without Scram Mitigating System Actuation Circuitry; and
The inspectors evaluated degraded performance issues involving the following  
    *       Rod Position Indication
risk-significant systems:  
    The inspectors reviewed events such as where ineffective equipment maintenance had
*  
    resulted in valid or invalid automatic actuations of engineered safeguards systems and
Nuclear Instrumentation;  
    independently verified the licensee's actions to address system performance or condition
*  
    problems in terms of the following:
Main Steam;
    *       implementing appropriate work practices;
*  
    *       identifying and addressing common cause failures;
Anticipated Transient Without Scram Mitigating System Actuation Circuitry; and  
    *       scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
*  
    *       characterizing system reliability issues for performance;
Rod Position Indication  
    *       charging unavailability for performance;
The inspectors reviewed events such as where ineffective equipment maintenance had  
    *       trending key parameters for condition monitoring;
resulted in valid or invalid automatic actuations of engineered safeguards systems and  
    *       ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
independently verified the licensee's actions to address system performance or condition  
    *       verifying appropriate performance criteria for SSCs/functions classified as (a)(2),
problems in terms of the following:  
              or appropriate and adequate goals and corrective actions for systems classified
*  
              as (a)(1).
implementing appropriate work practices;  
    The inspectors assessed performance issues with respect to the reliability, availability,
*  
    and condition monitoring of the system. In addition, the inspectors verified maintenance
identifying and addressing common cause failures;  
    effectiveness issues were entered into the CAP with the appropriate significance
*  
    characterization. Documents reviewed are listed in the Attachment to this report.
scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
    This inspection constituted four quarterly maintenance effectiveness samples as defined
*  
    in IP 71111.12-05.
characterizing system reliability issues for performance;  
  b. Findings
*  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
charging unavailability for performance;  
  a. Inspection Scope
*  
    The inspectors reviewed the licensee's evaluation and management of plant risk for the
trending key parameters for condition monitoring;  
    maintenance and emergent work activities affecting risk-significant and safety-related
*  
    equipment listed below to verify that the appropriate risk assessments were performed
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and  
    prior to removing equipment for work:
*  
    *       Rough lake conditions during emergent trash rack work;
verifying appropriate performance criteria for SSCs/functions classified as (a)(2),  
    *       Essential service water flow verification work concurrent with EDG testing; and
or appropriate and adequate goals and corrective actions for systems classified  
    *       Emergent repairs to the Unit 2 Motor-Driven Auxiliary Feedwater (MDAFW) pump
as (a)(1).  
              room ventilation unit
The inspectors assessed performance issues with respect to the reliability, availability,  
                                                15
and condition monitoring of the system. In addition, the inspectors verified maintenance  
effectiveness issues were entered into the CAP with the appropriate significance  
characterization. Documents reviewed are listed in the Attachment to this report.  
This inspection constituted four quarterly maintenance effectiveness samples as defined  
in IP 71111.12-05.  
b.  
Findings  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
a.  
Inspection Scope  
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
maintenance and emergent work activities affecting risk-significant and safety-related  
equipment listed below to verify that the appropriate risk assessments were performed  
prior to removing equipment for work:  
*  
Rough lake conditions during emergent trash rack work;  
*  
Essential service water flow verification work concurrent with EDG testing; and  
*  
Emergent repairs to the Unit 2 Motor-Driven Auxiliary Feedwater (MDAFW) pump  
room ventilation unit  


    These activities were selected based on their potential risk significance relative to the
    Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
16
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
    and complete. When emergent work was performed, the inspectors verified that the
These activities were selected based on their potential risk significance relative to the  
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that  
    of maintenance work, discussed the results of the assessment with the licensee's
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
and complete. When emergent work was performed, the inspectors verified that the  
    consistent with the risk assessment. The inspectors also reviewed TS requirements and
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
    walked down portions of redundant safety systems, when applicable, to verify risk
of maintenance work, discussed the results of the assessment with the licensee's  
    analysis assumptions were valid and applicable requirements were met.
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
    Documents reviewed during this inspection are listed in the Attachment to this report.
consistent with the risk assessment. The inspectors also reviewed TS requirements and  
    These maintenance risk assessments and emergent work control activities constituted
walked down portions of redundant safety systems, when applicable, to verify risk  
    three samples as defined in IP 71111.13-05.
analysis assumptions were valid and applicable requirements were met.  
  b. Findings
Documents reviewed during this inspection are listed in the Attachment to this report.
    No findings were identified.
These maintenance risk assessments and emergent work control activities constituted  
1R15 Operability Determinations and Functional Assessments (71111.15)
three samples as defined in IP 71111.13-05.  
  a. Inspection Scope
b.  
    The inspectors reviewed the following issues:
Findings  
    *       Main Steam Safety Valves lift during dual-unit trip;
No findings were identified.  
    *       Water intrusion into the Unit 1 TDAFW turbine bearings;
1R15 Operability Determinations and Functional Assessments (71111.15)  
    *       Question regarding TDAFW pump mission time;
a.  
    *       Inability to make new ice during the Unit 1 refueling outage;
Inspection Scope  
    *       Inadvertent placement of FME bag on AB Fuel Oil Storage Tank vent;
The inspectors reviewed the following issues:  
    *       Failure of automatic load tapping of Unit 2 Reserve Auxiliary Transformer and
*  
              failure of automatic generator trip during dual-unit trip; and
Main Steam Safety Valves lift during dual-unit trip;
    *       Leakby on a Unit 2 AFW flow control valve.
*  
    The inspectors selected these potential operability issues based on the risk significance
Water intrusion into the Unit 1 TDAFW turbine bearings;  
    of the associated components and systems. The inspectors evaluated the technical
*  
    adequacy of the evaluations to ensure that TS operability was properly justified and the
Question regarding TDAFW pump mission time;  
    subject component or system remained available such that no unrecognized increase in
*  
    risk occurred. The inspectors compared the operability and design criteria in the
Inability to make new ice during the Unit 1 refueling outage;  
    appropriate sections of the TS and UFSAR to the licensees evaluations to determine
*  
    whether the components or systems were operable. Where compensatory measures
Inadvertent placement of FME bag on AB Fuel Oil Storage Tank vent;  
    were required to maintain operability, the inspectors determined whether the measures
*  
    in place would function as intended and were properly controlled. The inspectors
Failure of automatic load tapping of Unit 2 Reserve Auxiliary Transformer and  
    determined, where appropriate, compliance with bounding limitations associated with the
failure of automatic generator trip during dual-unit trip; and  
    evaluations. Additionally, the inspectors reviewed a sampling of corrective action
*  
    documents to verify that the licensee was identifying and correcting any deficiencies
Leakby on a Unit 2 AFW flow control valve.  
    associated with operability evaluations. Documents reviewed are listed in the
The inspectors selected these potential operability issues based on the risk significance  
    Attachment to this report.
of the associated components and systems. The inspectors evaluated the technical  
    This operability inspection constituted seven samples as defined in IP 71111.15-05.
adequacy of the evaluations to ensure that TS operability was properly justified and the  
                                                16
subject component or system remained available such that no unrecognized increase in  
risk occurred. The inspectors compared the operability and design criteria in the  
appropriate sections of the TS and UFSAR to the licensees evaluations to determine  
whether the components or systems were operable. Where compensatory measures  
were required to maintain operability, the inspectors determined whether the measures  
in place would function as intended and were properly controlled. The inspectors  
determined, where appropriate, compliance with bounding limitations associated with the  
evaluations. Additionally, the inspectors reviewed a sampling of corrective action  
documents to verify that the licensee was identifying and correcting any deficiencies  
associated with operability evaluations. Documents reviewed are listed in the  
Attachment to this report.  
This operability inspection constituted seven samples as defined in IP 71111.15-05.  


b. Findings
(1) Failure to Identify Conditions Adverse to Quality Associated with the Unit 1 TDAFW
17
    Pump Turbine Oil System
    Introduction: A finding of very low safety significance (Green) with an associated NCV of
b.  
    10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the
Findings  
    inspectors for the licensees failure to promptly identify and correct a CAQ associated
(1) Failure to Identify Conditions Adverse to Quality Associated with the Unit 1 TDAFW  
    with Unit 1 TDAFW pump turbine bearing oil. Specifically, the licensee failed to identify
Pump Turbine Oil System  
    that water was entering the Unit 1 TDAFW pump turbine bearing oil system after leakage
Introduction: A finding of very low safety significance (Green) with an associated NCV of  
    had been identified directly above one of the TDAFW pump turbine bearings.
10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the  
    Description: On April 7, 2014, the licensee identified a 1 dpm leak from the Unit 1
inspectors for the licensees failure to promptly identify and correct a CAQ associated  
    TDAFW pump governor cooling pipe located directly above the outboard turbine bearing.
with Unit 1 TDAFW pump turbine bearing oil. Specifically, the licensee failed to identify  
    An AR was written (AR 2014-4473) which determined that due to the leak rate and the
that water was entering the Unit 1 TDAFW pump turbine bearing oil system after leakage  
    apparent lack of any equipment impacts, there were no operability concerns. On
had been identified directly above one of the TDAFW pump turbine bearings.  
    April 11, 2014, the licensee discovered that the turbine bearing oil level was
Description: On April 7, 2014, the licensee identified a 1 dpm leak from the Unit 1  
    approximately 0.5 inches above the MAXIMUM mark on the sight glass. Level had been
TDAFW pump governor cooling pipe located directly above the outboard turbine bearing.
    recorded in the logs as being within band for over a year without any prior evidence of
An AR was written (AR 2014-4473) which determined that due to the leak rate and the  
    high level. Additionally, there were no evolutions that had been performed which would
apparent lack of any equipment impacts, there were no operability concerns. On
    explain the high level. The licensee generated AR 2014-4684 to document this
April 11, 2014, the licensee discovered that the turbine bearing oil level was  
    condition. The AR documented several possible reasons for the unexplained level rise.
approximately 0.5 inches above the MAXIMUM mark on the sight glass. Level had been  
    One was that turbine building temperature had gone up. Another was that it was not
recorded in the logs as being within band for over a year without any prior evidence of  
    uncommon for personnel to unnecessarily add oil to the machine from time to time. No
high level. Additionally, there were no evolutions that had been performed which would  
    other information was provided to validate either potential cause. Additionally, there was
explain the high level. The licensee generated AR 2014-4684 to document this  
    no mention of the leak identified above one of the turbine bearings four days prior. No
condition. The AR documented several possible reasons for the unexplained level rise.
    formal monitoring plan was established. An action was created to sample the oil for
One was that turbine building temperature had gone up. Another was that it was not  
    water, but as of six weeks later, a work order had not been finalized and scheduled.
uncommon for personnel to unnecessarily add oil to the machine from time to time. No  
    The only other action was a lessons-learned that was created for Mechanical
other information was provided to validate either potential cause. Additionally, there was  
    Maintenance department regarding unnecessary oil adds. The response to the action
no mention of the leak identified above one of the turbine bearings four days prior. No  
    from the group was that they dont typically do oil adds, but that they discussed the topic
formal monitoring plan was established. An action was created to sample the oil for  
    anyway. The inspectors reviewed reference information with respect to oil levels and
water, but as of six weeks later, a work order had not been finalized and scheduled.  
    their importance to machine operability. According to the vendor manual, EPRI
The only other action was a lessons-learned that was created for Mechanical  
    guidance on Terry turbines, and an AR the licensee evaluated in 2012, oil level is
Maintenance department regarding unnecessary oil adds. The response to the action  
    extremely critical in the turbine bearing pedestals. The references all concluded that oil
from the group was that they dont typically do oil adds, but that they discussed the topic  
    level above the MAXIMUM mark could lead to oil frothing, which could affect stable
anyway. The inspectors reviewed reference information with respect to oil levels and  
    operation of the turbine and loss of oil from the system. Further, the references, along
their importance to machine operability. According to the vendor manual, EPRI  
    with the plant logs, stated that oil level should be kept at or slightly above the MINIMUM
guidance on Terry turbines, and an AR the licensee evaluated in 2012, oil level is  
    mark. Action Request 2014-4684 concluded that in April 2013, the reservoir was
extremely critical in the turbine bearing pedestals. The references all concluded that oil  
    over-filled to the MAXIMUM mark. No further information was provided on why this
level above the MAXIMUM mark could lead to oil frothing, which could affect stable  
    occurred or why it was acceptable to stay at the MAXIMUM mark. One quart of oil was
operation of the turbine and loss of oil from the system. Further, the references, along  
    drained from the turbine bearing pedestals, bringing the level back to near the
with the plant logs, stated that oil level should be kept at or slightly above the MINIMUM  
    MAXIMUM mark. Approximately five weeks later, an NRC inspector touring the plant
mark. Action Request 2014-4684 concluded that in April 2013, the reservoir was  
    questioned why level was near the MAXIMUM mark given a placard near the sight glass
over-filled to the MAXIMUM mark. No further information was provided on why this  
    said to keep level at the MINIMUM mark (which aligned with the references above).
occurred or why it was acceptable to stay at the MAXIMUM mark. One quart of oil was  
    The licensee generated an AR (2014-6315) about one week later on May 22 when the
drained from the turbine bearing pedestals, bringing the level back to near the  
    inspector asked about the condition again. In the AR, they documented the NRC
MAXIMUM mark. Approximately five weeks later, an NRC inspector touring the plant  
    observation and also the fact that an operator had noted level to be above the
questioned why level was near the MAXIMUM mark given a placard near the sight glass  
    MAXIMUM mark by approximately 0.25 inches. Oil was again drained from the
said to keep level at the MINIMUM mark (which aligned with the references above).
    machine, this time to right above the MINIMUM mark. The operability assessment
The licensee generated an AR (2014-6315) about one week later on May 22 when the  
    (which was not documented until the following day), stated that at time of discovery, the
inspector asked about the condition again. In the AR, they documented the NRC  
                                                17
observation and also the fact that an operator had noted level to be above the  
MAXIMUM mark by approximately 0.25 inches. Oil was again drained from the  
machine, this time to right above the MINIMUM mark. The operability assessment  
(which was not documented until the following day), stated that at time of discovery, the  


machine was operable because of oil level not affecting operability of the turbine and a
history of overfilling that sometimes required draining of the oil. Further, a statement
18
was made that there had been a consistent oil level trend for the past month. Again,
the leakage above the bearing was not discussed. There was no discussion of the
machine was operable because of oil level not affecting operability of the turbine and a  
previous high-level condition from April 11. On May 23, the licensee decided to
history of overfilling that sometimes required draining of the oil. Further, a statement  
completely drain the oil and sample it for water; 620 ml of water was found in the 2.5
was made that there had been a consistent oil level trend for the past month. Again,
gallon system. New oil was added, and an apparent cause evaluation was performed.
the leakage above the bearing was not discussed. There was no discussion of the  
The evaluation concluded that leakage above the bearing housing (documented
previous high-level condition from April 11. On May 23, the licensee decided to  
originally in AR 2014-4473), combined with a small casing steam leak that condensed
completely drain the oil and sample it for water; 620 ml of water was found in the 2.5  
above the housing while the machine was in operation, caused the water intrusion in the
gallon system. New oil was added, and an apparent cause evaluation was performed.
bearing oil. Later evaluation determined the leak rate from the pipe had increased to
The evaluation concluded that leakage above the bearing housing (documented  
8 dpm in standby, and while running the leak rate was 20 dpm. The leakage sources
originally in AR 2014-4473), combined with a small casing steam leak that condensed  
were diverted away from the bearing housing with a temporary modification pending
above the housing while the machine was in operation, caused the water intrusion in the  
repairs (which were completed in the September-October 2014 refueling outage).
bearing oil. Later evaluation determined the leak rate from the pipe had increased to  
Based on the above, the inspectors concluded the licensee had sufficient information to
8 dpm in standby, and while running the leak rate was 20 dpm. The leakage sources  
promptly identify and correct water intrusion into the TDAFW turbine bearing oil system
were diverted away from the bearing housing with a temporary modification pending  
on April 11 and May 22, 2014. Additionally, the licensee failed to identify the potential
repairs (which were completed in the September-October 2014 refueling outage).
operability impacts (as described in the multiple references above) on April 11 and
Based on the above, the inspectors concluded the licensee had sufficient information to  
May 22 when oil level was above the MAXIMUM mark. Water intrusion into safety-
promptly identify and correct water intrusion into the TDAFW turbine bearing oil system  
related oil systems is a CAQ.
on April 11 and May 22, 2014. Additionally, the licensee failed to identify the potential  
Analysis: The failure to promptly identify and correct a CAQ, as required by
operability impacts (as described in the multiple references above) on April 11 and
10 CFR Part 50, Appendix B, Criterion 16, associated with water intrusion into the
May 22 when oil level was above the MAXIMUM mark. Water intrusion into safety-
TDAFW turbine oil system was an issue warranting further review in the SDP. Per
related oil systems is a CAQ.  
IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, the issue was
Analysis: The failure to promptly identify and correct a CAQ, as required by
more-than-minor because it adversely affected the Configuration Control attribute of the
10 CFR Part 50, Appendix B, Criterion 16, associated with water intrusion into the  
Mitigating Systems Cornerstone, whose objective is to ensure the availability, reliability,
TDAFW turbine oil system was an issue warranting further review in the SDP. Per
and capability of systems that respond to initiating events to prevent undesirable
IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, the issue was  
consequences. Additionally, if left uncorrected, the issue could lead to a more significant
more-than-minor because it adversely affected the Configuration Control attribute of the  
safety concern. Specifically, not recognizing water intrusion into safety-related oil
Mitigating Systems Cornerstone, whose objective is to ensure the availability, reliability,  
systems can impact operability and affect how safety equipment operates.
and capability of systems that respond to initiating events to prevent undesirable  
The inspectors assessed the finding for significance using IMC 0609, Significance
consequences. Additionally, if left uncorrected, the issue could lead to a more significant  
Determination Process, issued June 2, 2012. Per Appendix A, The Significance
safety concern. Specifically, not recognizing water intrusion into safety-related oil  
Determination Process (SDP) for Findings-at-Power, issued June 19, 2012, the finding
systems can impact operability and affect how safety equipment operates.  
screened as Green, or very low safety significance, in Exhibit 2. Specifically, all
The inspectors assessed the finding for significance using IMC 0609, Significance  
questions were answered no under Section A for findings related to Mitigating SSCs
Determination Process, issued June 2, 2012. Per Appendix A, The Significance  
and Functionality. The inspectors reviewed the licensees past operability evaluation
Determination Process (SDP) for Findings-at-Power, issued June 19, 2012, the finding  
and concluded that given the projected amount of water that could be entrained in the oil
screened as Green, or very low safety significance, in Exhibit 2. Specifically, all  
during operation, along with the duration of operation assumed in the safety analyses,
questions were answered no under Section A for findings related to Mitigating SSCs  
that operability of the pump would be maintained.
and Functionality. The inspectors reviewed the licensees past operability evaluation  
The inspectors determined the finding had an associated cross-cutting aspect in the
and concluded that given the projected amount of water that could be entrained in the oil  
Human Performance area, specifically, H.11, Challenge the Unknown. Some of the
during operation, along with the duration of operation assumed in the safety analyses,  
tenets of H.11, as described in NUREG-2165, Safety Culture Common Language
that operability of the pump would be maintained.  
Initiative, Section QA.2, Questioning Attitude, are that individuals avoid complacency
The inspectors determined the finding had an associated cross-cutting aspect in the  
and continuously challenge existing conditions in order to identify discrepancies that
Human Performance area, specifically, H.11, Challenge the Unknown. Some of the  
might result in error or inappropriate action. Further, it states that individuals challenge
tenets of H.11, as described in NUREG-2165, Safety Culture Common Language  
unanticipated results rather than rationalize them, and that abnormal indications are not
Initiative, Section QA.2, Questioning Attitude, are that individuals avoid complacency  
attributed to indication problems. Regarding the TDAFW oil system, the licensee
and continuously challenge existing conditions in order to identify discrepancies that  
rationalized why the level was increasing without sufficient investigation given the
might result in error or inappropriate action. Further, it states that individuals challenge  
                                          18
unanticipated results rather than rationalize them, and that abnormal indications are not  
attributed to indication problems. Regarding the TDAFW oil system, the licensee  
rationalized why the level was increasing without sufficient investigation given the  


    significance of the system, and did not seek further information that was readily available
    regarding appropriate oil levels.
19
    Enforcement: 10 CFR Part 50, Appendix B, Criterion 16, Corrective Action, requires, in
    part, that conditions adverse to quality, such as deficiencies, defective material and
significance of the system, and did not seek further information that was readily available  
    equipment, and nonconformances are promptly identified and corrected.
regarding appropriate oil levels.  
    Contrary to the above, between April 11 and May 23, 2014, the licensee failed to
Enforcement: 10 CFR Part 50, Appendix B, Criterion 16, Corrective Action, requires, in  
    promptly identify and correct a CAQ. Specifically, the licensee failed to promptly identify
part, that conditions adverse to quality, such as deficiencies, defective material and  
    and correct water intrusion into the safety-related Unit 1 TDAFW pump oil system
equipment, and nonconformances are promptly identified and corrected.
    despite multiple opportunities to do so. On April 7, the licensee became aware of a
Contrary to the above, between April 11 and May 23, 2014, the licensee failed to  
    water leak directly above the TDAFW pump turbine outboard bearing. On April 11, and
promptly identify and correct a CAQ. Specifically, the licensee failed to promptly identify  
    May 22, the licensee learned that the oil level had exceeded the MAXIMUM mark. The
and correct water intrusion into the safety-related Unit 1 TDAFW pump oil system  
    actions taken (draining the oil level) did not correct the condition adverse to quality in
despite multiple opportunities to do so. On April 7, the licensee became aware of a  
    that water continued to leak into the oil. On May 23, the licensee drained the oil system
water leak directly above the TDAFW pump turbine outboard bearing. On April 11, and  
    and discovered approximately 620 ml of water.
May 22, the licensee learned that the oil level had exceeded the MAXIMUM mark. The  
    For immediate corrective actions, the licensee added new oil to the system and installed
actions taken (draining the oil level) did not correct the condition adverse to quality in  
    a temporary modification to prevent further water intrusion. Further corrective actions
that water continued to leak into the oil. On May 23, the licensee drained the oil system  
    included an apparent cause evaluation and past operability evaluation. Permanent
and discovered approximately 620 ml of water.  
    repairs to the cooling water leak above the bearing were completed during the Fall 2014
For immediate corrective actions, the licensee added new oil to the system and installed  
    refueling outage. The licensee initiated AR-2014-6315 to document the condition and
a temporary modification to prevent further water intrusion. Further corrective actions  
    track corrective actions.
included an apparent cause evaluation and past operability evaluation. Permanent  
    This violation is being treated as an NCV, consistent with Section 2.3.2 of the
repairs to the cooling water leak above the bearing were completed during the Fall 2014  
    Enforcement Policy because it was of very low safety significance and was entered into
refueling outage. The licensee initiated AR-2014-6315 to document the condition and  
    the licensees CAP. (NCV 05000315/2014005-01; Failure to Identify Conditions
track corrective actions.  
    Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil System)
This violation is being treated as an NCV, consistent with Section 2.3.2 of the  
(2) Unplanned Inoperability of the AB Fuel Oil Storage Tank During Maintenance
Enforcement Policy because it was of very low safety significance and was entered into  
    Introduction: A finding of very low safety significance (Green) with an associated NCV of
the licensees CAP. (NCV 05000315/2014005-01; Failure to Identify Conditions  
    TS 5.4, Procedures, was self-revealed when a vacuum was inadvertently drawn on the
Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil System)  
    AB FOST during preparations for surveillance activities. The vacuum caused an
(2) Unplanned Inoperability of the AB Fuel Oil Storage Tank During Maintenance  
    indication of lowering level in the tank, alarms, and an unplanned TS LCO action
Introduction: A finding of very low safety significance (Green) with an associated NCV of  
    statement entry.
TS 5.4, Procedures, was self-revealed when a vacuum was inadvertently drawn on the  
    Description: On August 20, 2014, the licensee was performing work activities in
AB FOST during preparations for surveillance activities. The vacuum caused an  
    preparation for an upcoming, routine leak-test of the AB FOST. The AB FOST is one of
indication of lowering level in the tank, alarms, and an unplanned TS LCO action  
    two underground tanks on site that supply fuel to the EDGs via the smaller day tanks
statement entry.  
    (which are provided for each EDG and offer a more limited, immediate fuel supply). The
Description: On August 20, 2014, the licensee was performing work activities in  
    test consists of establishing a vacuum in the tank and monitoring it for a period of time.
preparation for an upcoming, routine leak-test of the AB FOST. The AB FOST is one of  
    Several support activities are required to be performed prior to the test, some of which
two underground tanks on site that supply fuel to the EDGs via the smaller day tanks  
    include transfer of fuel from the FOST to the day tanks, removal of a vent cover for the
(which are provided for each EDG and offer a more limited, immediate fuel supply). The  
    FOST, and connection of vendor-supplied vacuum and test equipment to the vent. Per
test consists of establishing a vacuum in the tank and monitoring it for a period of time.
    the overarching surveillance procedure, the basic order of activities should have been to
Several support activities are required to be performed prior to the test, some of which  
    loosen the vent cover, transfer an amount of fuel to the day tanks, remove the FOST
include transfer of fuel from the FOST to the day tanks, removal of a vent cover for the  
    from service, remove the vent cover, hook up the test equipment, and perform the test.
FOST, and connection of vendor-supplied vacuum and test equipment to the vent. Per  
    During the day shift on August 20, workers went out to work on the vent cover. The
the overarching surveillance procedure, the basic order of activities should have been to  
    associated work instruction did not provide adequate guidance on what exactly was to
loosen the vent cover, transfer an amount of fuel to the day tanks, remove the FOST  
    be done. While the intent was just to loosen the cover at that point, the Subject of the
from service, remove the vent cover, hook up the test equipment, and perform the test.
                                              19
During the day shift on August 20, workers went out to work on the vent cover. The  
associated work instruction did not provide adequate guidance on what exactly was to  
be done. While the intent was just to loosen the cover at that point, the Subject of the  


WO was Remove manway cover and vent cover. The instructions in the WO were
written as loosen/remove vent cover, and under the Precautions section the statement
20
Per tank procedure, as a minimum, we only have to loosen vent filter. The workers
ended up removing the cover instead of loosening it, and placed an FME bag over the
WO was Remove manway cover and vent cover. The instructions in the WO were  
vent to prevent foreign material from entering the tank. Later on night shift, operations
written as loosen/remove vent cover, and under the Precautions section the statement  
staff commenced the transfer of fuel to the day tanks. With the FME bag installed, a
Per tank procedure, as a minimum, we only have to loosen vent filter. The workers  
vacuum was drawn on the tank. Based on the configuration of the level instruments and
ended up removing the cover instead of loosening it, and placed an FME bag over the  
tank vent, the instruments indicated a lowering tank level and generated low level alarms
vent to prevent foreign material from entering the tank. Later on night shift, operations  
because of the vacuum. Operators performed a back-up measurement of tank level
staff commenced the transfer of fuel to the day tanks. With the FME bag installed, a  
using a dip stick, however, again, based on the tank construction, this method also
vacuum was drawn on the tank. Based on the configuration of the level instruments and  
showed what appeared to be a lowering tank level. With this information, operators
tank vent, the instruments indicated a lowering tank level and generated low level alarms  
believed an actual loss of fuel from the tank had occurred. Absent any indications in the
because of the vacuum. Operators performed a back-up measurement of tank level  
plant of fuel leaving the system, they concluded a release to the environment may have
using a dip stick, however, again, based on the tank construction, this method also  
occurred. Appropriate reports were made to state, federal, and local agencies.
showed what appeared to be a lowering tank level. With this information, operators  
Additionally, the operators entered TS LCO 3.8.3 Condition A based on the observed
believed an actual loss of fuel from the tank had occurred. Absent any indications in the  
level indications. During investigation soon after the abnormal level indications, the FME
plant of fuel leaving the system, they concluded a release to the environment may have  
bag was found on the vent. Once removed, level in the tank returned to normal. There
occurred. Appropriate reports were made to state, federal, and local agencies.
was no actual loss of fuel from the tank.
Additionally, the operators entered TS LCO 3.8.3 Condition A based on the observed  
Analysis: The failure to have adequate instructions for performing work on safety-related
level indications. During investigation soon after the abnormal level indications, the FME  
equipment, as required by TS 5.4, Procedures, was a performance deficiency
bag was found on the vent. Once removed, level in the tank returned to normal. There  
warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued
was no actual loss of fuel from the tank.  
September 7, 2012. The performance deficiency was more than minor because it
Analysis: The failure to have adequate instructions for performing work on safety-related  
adversely impacted the Configuration Control attribute of the Mitigating Systems
equipment, as required by TS 5.4, Procedures, was a performance deficiency  
cornerstone, whose objective is ensuring the availability, reliability, and capability of
warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued  
systems that respond to initiating events to prevent undesirable consequences.
September 7, 2012. The performance deficiency was more than minor because it  
The finding screened as Green, or very low safety significance, utilizing IMC 0609
adversely impacted the Configuration Control attribute of the Mitigating Systems  
Appendix A, The Significance Determination Process for Findings at Power, issued
cornerstone, whose objective is ensuring the availability, reliability, and capability of  
June 19, 2012. Specifically, all questions were answered no under Section A of
systems that respond to initiating events to prevent undesirable consequences.  
Exhibit 2 for Mitigating Systems, since that was the affected cornerstone. The FME bag
The finding screened as Green, or very low safety significance, utilizing IMC 0609  
was installed, which rendered the AB FOST inoperable, for approximately 16 hours.
Appendix A, The Significance Determination Process for Findings at Power, issued  
This was less than the TS allowed outage time of 48 hours.
June 19, 2012. Specifically, all questions were answered no under Section A of
The finding had an associated cross-cutting aspect in the human performance area,
Exhibit 2 for Mitigating Systems, since that was the affected cornerstone. The FME bag  
specifically, H.5, Work Management. Work activities should be planned, controlled, and
was installed, which rendered the AB FOST inoperable, for approximately 16 hours.
executed with nuclear safety as the overriding priority. Contrary to the tenets of the
This was less than the TS allowed outage time of 48 hours.  
cross-cutting aspect, the work was planned and executed with inadequate work
The finding had an associated cross-cutting aspect in the human performance area,  
instructions. Further, there was a lack of coordination between a number of work groups
specifically, H.5, Work Management. Work activities should be planned, controlled, and  
and activities associated with the test.
executed with nuclear safety as the overriding priority. Contrary to the tenets of the  
Enforcement: Technical Specification 5.4, Procedures, states, in part, that written
cross-cutting aspect, the work was planned and executed with inadequate work  
procedures shall be established, implemented, and maintained covering the applicable
instructions. Further, there was a lack of coordination between a number of work groups  
procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in
and activities associated with the test.  
part, that maintenance that can affect the performance of safety-related equipment
Enforcement: Technical Specification 5.4, Procedures, states, in part, that written  
should be properly preplanned and performed in accordance with written procedures,
procedures shall be established, implemented, and maintained covering the applicable  
documented instructions, or drawings appropriate to the circumstances.
procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in  
Contrary to those requirements, on August 20, 2014, the AB FOST leak test was
part, that maintenance that can affect the performance of safety-related equipment  
performed with inadequate procedures and with tasks done outside the proper
should be properly preplanned and performed in accordance with written procedures,  
                                        20
documented instructions, or drawings appropriate to the circumstances.  
Contrary to those requirements, on August 20, 2014, the AB FOST leak test was  
performed with inadequate procedures and with tasks done outside the proper  


    sequence. As a result, the AB FOST was rendered inoperable for approximately
    16 hours.
21
    Immediate corrective actions involved the removal of an FME bag which had been
    placed over the AB FOST vent. The licensee also generated AR-2014-9877, which
sequence. As a result, the AB FOST was rendered inoperable for approximately
    included a root cause analysis. This violation is being treated as an NCV, consistent
16 hours.  
    with Section 2.3.2 of the Enforcement Policy because it was of very low safety
Immediate corrective actions involved the removal of an FME bag which had been  
    significance and was entered into the licensees CAP. (NCV 05000315/2014005-02;
placed over the AB FOST vent. The licensee also generated AR-2014-9877, which  
    05000316/2014005-02; Unplanned Inoperability of the AB Fuel Oil Storage Tank
included a root cause analysis. This violation is being treated as an NCV, consistent  
    During Maintenance)
with Section 2.3.2 of the Enforcement Policy because it was of very low safety  
1R18 Plant Modifications (71111.18)
significance and was entered into the licensees CAP. (NCV 05000315/2014005-02;  
  a. Inspection Scope
05000316/2014005-02; Unplanned Inoperability of the AB Fuel Oil Storage Tank  
    The inspectors reviewed the following modification(s):
During Maintenance)  
    *       Permanent removal of shield/missile blocks
1R18 Plant Modifications (71111.18)  
    The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety
a.  
    evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to
Inspection Scope  
    verify that the modification did not affect the operability or availability of the affected
The inspectors reviewed the following modification(s):  
    system(s). The inspectors, as applicable, observed ongoing and completed work
*  
    activities to ensure that the modifications were installed as directed and consistent with
Permanent removal of shield/missile blocks  
    the design control documents; the modifications operated as expected; post-modification
The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety  
    testing adequately demonstrated continued system operability, availability, and reliability;
evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to  
    and that operation of the modifications did not impact the operability of any interfacing
verify that the modification did not affect the operability or availability of the affected  
    systems. As applicable, the inspectors verified that relevant procedure, design, and
system(s). The inspectors, as applicable, observed ongoing and completed work  
    licensing documents were properly updated. Lastly, the inspectors discussed the plant
activities to ensure that the modifications were installed as directed and consistent with  
    modification with operations, engineering, and training personnel to ensure that the
the design control documents; the modifications operated as expected; post-modification  
    individuals were aware of how the operation with the plant modification in place could
testing adequately demonstrated continued system operability, availability, and reliability;  
    impact overall plant performance. Documents reviewed are listed in the Attachment to
and that operation of the modifications did not impact the operability of any interfacing  
    this report.
systems. As applicable, the inspectors verified that relevant procedure, design, and  
    This inspection constituted one permanent plant modification sample as defined in
licensing documents were properly updated. Lastly, the inspectors discussed the plant  
    IP 71111.18-05.
modification with operations, engineering, and training personnel to ensure that the  
  b. Findings
individuals were aware of how the operation with the plant modification in place could  
    Lack of Adequate Design Review of Effects of Removing the Auxiliary Missile Blocks
impact overall plant performance. Documents reviewed are listed in the Attachment to  
    from the Containment Accident Shield
this report.  
    Introduction: A finding of very-low safety significance (Green) and associated NCV of
This inspection constituted one permanent plant modification sample as defined in  
    Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, was identified by the
IP 71111.18-05.  
    NRC inspectors for the licensees inadequate radiological review of permanently
b.  
    removing the AMBs from the Unit 1 and Unit 2 containment accident shields.
Findings  
    Description: In March 2014, the NRC reviewed a licensee modification
Lack of Adequate Design Review of Effects of Removing the Auxiliary Missile Blocks  
    (EC-0000049191) to the Unit 1 and 2 safety-related containment accident shields. The
from the Containment Accident Shield  
    modification consisted of permanently removing the AMBs, located in front of the primary
Introduction: A finding of very-low safety significance (Green) and associated NCV of  
    containment equipment hatches on the 650 elevation of the Auxiliary Building. The
Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, was identified by the  
    AMBs are portable and removable shield blocks and are a part of the safety-related
NRC inspectors for the licensees inadequate radiological review of permanently  
                                              21
removing the AMBs from the Unit 1 and Unit 2 containment accident shields.  
Description: In March 2014, the NRC reviewed a licensee modification  
(EC-0000049191) to the Unit 1 and 2 safety-related containment accident shields. The  
modification consisted of permanently removing the AMBs, located in front of the primary  
containment equipment hatches on the 650 elevation of the Auxiliary Building. The  
AMBs are portable and removable shield blocks and are a part of the safety-related  


containment accident shield. The AMBs are in place during power operations for
shielding purposes. The AMBs are removed during plant outages to permit containment
22
access for equipment.
The main purpose of the accident shield, as a part of original plant design and currently
containment accident shield. The AMBs are in place during power operations for  
described in the UFSAR, Section 11.2.1.1.4, is to ensure safe radiation levels outside
shielding purposes. The AMBs are removed during plant outages to permit containment  
the containment building following a maximum design-basis accident; specifically, a
access for equipment.  
large break loss-of-coolant accident (LBLOCA). The plant containment and the accident
The main purpose of the accident shield, as a part of original plant design and currently  
shield function (USFAR Section 11.2.1) ensure that operating personnel at the plant and
described in the UFSAR, Section 11.2.1.1.4, is to ensure safe radiation levels outside  
the general public are protected by adequate containment shielding, post LBLOCA. This
the containment building following a maximum design-basis accident; specifically, a  
was in accordance with plant specific design Criteria 1 of 10 CFR Part 50 General
large break loss-of-coolant accident (LBLOCA). The plant containment and the accident  
Design Criteria 1 Quality Standards and Records of Appendix A General Design
shield function (USFAR Section 11.2.1) ensure that operating personnel at the plant and  
Criteria for Nuclear Power Plants, 10 CFR Part 20 Standards for Protection Against
the general public are protected by adequate containment shielding, post LBLOCA. This  
Radiation, and 10 CFR Part 100 Reactor Site Criteria. The inspectors reviewed the
was in accordance with plant specific design Criteria 1 of 10 CFR Part 50 General  
original and current plant design configuration and determined that, prior to plant
Design Criteria 1 Quality Standards and Records of Appendix A General Design  
modification (EC-0000049191), the plant design met General Design Criteria 1 for
Criteria for Nuclear Power Plants, 10 CFR Part 20 Standards for Protection Against  
radiation safety. Specifically, RG 1.69 Concrete Radiation Shields for Nuclear Power
Radiation, and 10 CFR Part 100 Reactor Site Criteria. The inspectors reviewed the  
Plants was explicit in stating that General Design Criteria 1 for containment ensures
original and current plant design configuration and determined that, prior to plant  
reasonable assurance for compliance to 10 CFR Part 20 Standards for Protection
modification (EC-0000049191), the plant design met General Design Criteria 1 for  
Against Radiation under post-accident conditions. Additionally, initial plant design for
radiation safety. Specifically, RG 1.69 Concrete Radiation Shields for Nuclear Power  
the containment accident shield was consistent with RG 1.69 Concrete Radiation
Plants was explicit in stating that General Design Criteria 1 for containment ensures  
Shields for Nuclear Power Plants.
reasonable assurance for compliance to 10 CFR Part 20 Standards for Protection  
Using the licensees design basis source term, licensee calculation number RS-C-0046
Against Radiation under post-accident conditions. Additionally, initial plant design for  
Doses and Dose Rates from Post LOCA Airborne Sources determined that with the
the containment accident shield was consistent with RG 1.69 Concrete Radiation  
AMBs in place, the Post LBLOCA dose rates were:
Shields for Nuclear Power Plants.  
    * A nominal 31 Rem/hr at 1 second after LBLOCA at 1 inch from the AMBs; and
Using the licensees design basis source term, licensee calculation number RS-C-0046  
    * A nominal 3.9 Rem/hr at 1 second after LBLOCA at 50 feet from the AMBs.
Doses and Dose Rates from Post LOCA Airborne Sources determined that with the  
These dose rates provide for safe radiation levels outside the containment building
AMBs in place, the Post LBLOCA dose rates were:  
following a maximum design-basis accident consistent with the UFSAR design
*  
statements and in accordance with the requirements of 10 CFR Part 20, Standards for
A nominal 31 Rem/hr at 1 second after LBLOCA at 1 inch from the AMBs; and
Protection Against Radiation.
*  
The licensee provided no comparable post-modification dose rate calculations to the
A nominal 3.9 Rem/hr at 1 second after LBLOCA at 50 feet from the AMBs.
inspectors specific to AB 650 elevation once the AMBs were removed. However, the
These dose rates provide for safe radiation levels outside the containment building  
licensee provided information (Calculation Number RS-C-0232, Equipment Hatch Dose
following a maximum design-basis accident consistent with the UFSAR design  
Rates - Gap Release; Revision 01) that showed calculated Post LBLOCA dose rates
statements and in accordance with the requirements of 10 CFR Part 20, Standards for  
of 196.2 Rem/hr at 45 feet from the equipment hatch. Additionally, the licensee had
Protection Against Radiation.  
analogous Post-LBLOCA dose rate calculations for the containment personnel hatch.
The licensee provided no comparable post-modification dose rate calculations to the  
These dose rates provide a frame of reference, in that, the calculations provide for no
inspectors specific to AB 650 elevation once the AMBs were removed. However, the  
AMB shielding. However, the calculations did include shielding benefit from the inside
licensee provided information (Calculation Number RS-C-0232, Equipment Hatch Dose  
containment crane wall (Calculation Number RS-C-0046, Doses and Dose Rates from
Rates - Gap Release; Revision 01) that showed calculated Post LBLOCA dose rates
Post LOCA Airborne Sources). Specific calculated dose rates were:
of 196.2 Rem/hr at 45 feet from the equipment hatch. Additionally, the licensee had  
*   A nominal 36,300 Rem/hr at 1 second after LBLOCA at 1 inch from the personnel
analogous Post-LBLOCA dose rate calculations for the containment personnel hatch.
    hatch; and
These dose rates provide a frame of reference, in that, the calculations provide for no  
*   A nominal 397 Rem/hr at 1 second after LBLOCA at 50 feet from the personnel
AMB shielding. However, the calculations did include shielding benefit from the inside  
    hatch.
containment crane wall (Calculation Number RS-C-0046, Doses and Dose Rates from  
                                        22
Post LOCA Airborne Sources). Specific calculated dose rates were:  
*  
A nominal 36,300 Rem/hr at 1 second after LBLOCA at 1 inch from the personnel  
hatch; and  
*  
A nominal 397 Rem/hr at 1 second after LBLOCA at 50 feet from the personnel  
hatch.


The inspectors determined that post-modification dose rates on the AB 650 elevation
could result in lethal doses, as defined in NUREG/CR 6545 Probabilistic Accident
23
Consequence Uncertainty Analysis: Early Health Effects Uncertainty Assessment, to
individuals in a very short period of time (from fractions of a second to minutes,
The inspectors determined that post-modification dose rates on the AB 650 elevation  
depending on the location of personnel relative to the radiation source). By permanently
could result in lethal doses, as defined in NUREG/CR 6545 Probabilistic Accident  
removing the AMBs, the licensee failed to provide for safe radiation levels outside the
Consequence Uncertainty Analysis: Early Health Effects Uncertainty Assessment, to  
containment building following a maximum design-basis accident, contrary to the design
individuals in a very short period of time (from fractions of a second to minutes,  
bases and inconsistent with the requirements of 10 CFR Part 20.
depending on the location of personnel relative to the radiation source). By permanently  
Additionally, 10 CFR 20.1101(b) and RG 1.69 state, in part, that the licensee shall use,
removing the AMBs, the licensee failed to provide for safe radiation levels outside the  
to the extent practical, engineering controls based upon sound radiation principles to
containment building following a maximum design-basis accident, contrary to the design  
achieve occupational doses and doses to members of the public that are
bases and inconsistent with the requirements of 10 CFR Part 20.  
as-low-as-reasonably-achievable (ALARA). Original plant design and the plants 40-year
Additionally, 10 CFR 20.1101(b) and RG 1.69 state, in part, that the licensee shall use,  
operational history demonstrate that plant operation with the AMBs in place was both
to the extent practical, engineering controls based upon sound radiation principles to  
practical and ALARA.
achieve occupational doses and doses to members of the public that are  
The licensee documented this issue in the CAP as AR 2014-13016. Corrective actions
as-low-as-reasonably-achievable (ALARA). Original plant design and the plants 40-year  
included licensee determination to achieve radiation attenuation analogous to original
operational history demonstrate that plant operation with the AMBs in place was both  
plant design of the AMBs in place.
practical and ALARA.  
Analysis: The inspectors determined that the licensees inadequate radiological review
The licensee documented this issue in the CAP as AR 2014-13016. Corrective actions  
of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident
included licensee determination to achieve radiation attenuation analogous to original  
shields was a performance deficiency. The performance deficiency was determined to
plant design of the AMBs in place.  
be more than minor (Green) because it was associated with the Barrier Integrity
Analysis: The inspectors determined that the licensees inadequate radiological review  
Cornerstone attribute of design control; and adversely affected the cornerstone objective
of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident  
of maintaining radiological barrier functionality of the safety-related containment accident
shields was a performance deficiency. The performance deficiency was determined to  
shield. Specifically, the failure to control plant design and adequately evaluate the
be more than minor (Green) because it was associated with the Barrier Integrity  
radiological effects of permanently removing the AMBs from the Unit 1 and Unit 2
Cornerstone attribute of design control; and adversely affected the cornerstone objective  
containment accident shields did not ensure that the accident shield will provide its
of maintaining radiological barrier functionality of the safety-related containment accident  
design function to ensure safe radiation levels outside the containment building following
shield. Specifically, the failure to control plant design and adequately evaluate the  
a maximum design basis accident.
radiological effects of permanently removing the AMBs from the Unit 1 and Unit 2  
The inspectors evaluated the finding using the SDP in accordance with IMC 0609,
containment accident shields did not ensure that the accident shield will provide its  
Significance Determination Process, Attachment 0609.04, Initial Characterization of
design function to ensure safe radiation levels outside the containment building following  
Findings, dated June 19, 2012. Because the finding impacted the Barrier Integrity
a maximum design basis accident.  
Cornerstone, the inspectors screened the finding through IMC 0609, Appendix A, The
The inspectors evaluated the finding using the SDP in accordance with IMC 0609,  
Significance Determination Process for Findings At-Power, dated June 19, 2012, using
Significance Determination Process, Attachment 0609.04, Initial Characterization of  
Exhibit 3, Barrier Integrity Screening Questions. The finding screened as of very-low
Findings, dated June 19, 2012. Because the finding impacted the Barrier Integrity  
safety significance (Green) because the finding only represented a degradation of the
Cornerstone, the inspectors screened the finding through IMC 0609, Appendix A, The  
radiological barrier function provided for the Auxiliary Building.
Significance Determination Process for Findings At-Power, dated June 19, 2012, using  
The inspectors determined the cause of this finding did not represent current licensee
Exhibit 3, Barrier Integrity Screening Questions. The finding screened as of very-low  
performance and, thus, no cross-cutting aspect was assigned.
safety significance (Green) because the finding only represented a degradation of the  
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, requires,
radiological barrier function provided for the Auxiliary Building.  
in part, that design changes be subject to design control measures commensurate with
The inspectors determined the cause of this finding did not represent current licensee  
those applied to the original design.
performance and, thus, no cross-cutting aspect was assigned.  
Contrary to the above, on February 6, 2009, the licensee performed a design change
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, requires,  
and failed to subject it to design control measures commensurate with those applied to
in part, that design changes be subject to design control measures commensurate with  
the original design. Specifically, the licensee modified the original plant design by
those applied to the original design.  
                                          23
Contrary to the above, on February 6, 2009, the licensee performed a design change  
and failed to subject it to design control measures commensurate with those applied to  
the original design. Specifically, the licensee modified the original plant design by  


    removing the auxiliary missile blocks from the safety-related accident shield. However,
    the design control measures applied to the modification failed to ensure safe radiation
24
    levels outside the containment accident shield following a design basis loss-of-coolant
    accident.
removing the auxiliary missile blocks from the safety-related accident shield. However,  
    Because this violation was of very-low safety significance and was entered into the
the design control measures applied to the modification failed to ensure safe radiation  
    licensees CAP (AR 2014-13016), this violation is being treated as an NCV, consistent
levels outside the containment accident shield following a design basis loss-of-coolant  
    with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000315/2014005-03;
accident.  
    05000316/2014005-03; Radiological Impact of the Removal of the Auxiliary Shield
Because this violation was of very-low safety significance and was entered into the  
    Blocks on the Containment Accident Shield Post LBLOCA)
licensees CAP (AR 2014-13016), this violation is being treated as an NCV, consistent  
1R19 Post-Maintenance Testing (71111.19)
with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000315/2014005-03;  
  a. Inspection Scope
05000316/2014005-03; Radiological Impact of the Removal of the Auxiliary Shield  
    The inspectors reviewed the following post-maintenance activities to verify that
Blocks on the Containment Accident Shield Post LBLOCA)  
    procedures and test activities were adequate to ensure system operability and functional
1R19 Post-Maintenance Testing (71111.19)  
    capability:
a.  
    *       Unit 1 AB EDG following governor replacement;
Inspection Scope  
    *       Unit 1 CRID III and IV maintenance;
The inspectors reviewed the following post-maintenance activities to verify that  
    *       Unit 2 UAT breakers following failure to close;
procedures and test activities were adequate to ensure system operability and functional  
    *       Unit 1 CD EDG governor replacement and aftercooler maintenance;
capability:  
    *       Unit 1 TDAFW governor overhaul;
*  
    *       Repair of Unit 2 AFW flow control valve flow retention issue;
Unit 1 AB EDG following governor replacement;  
    *       Repair of circuitry associated with failure of fast transfer and generator trip during
*  
            dual-unit trip; and
Unit 1 CRID III and IV maintenance;  
    *       Unit 1 TDAFW repairs following inadvertent trip.
*  
    These activities were selected based upon the structure, system, or component's ability
Unit 2 UAT breakers following failure to close;  
    to impact risk. The inspectors evaluated these activities for the following (as applicable):
*  
    the effect of testing on the plant had been adequately addressed; testing was adequate
Unit 1 CD EDG governor replacement and aftercooler maintenance;  
    for the maintenance performed; acceptance criteria were clear and demonstrated
*  
    operational readiness; test instrumentation was appropriate; tests were performed as
Unit 1 TDAFW governor overhaul;  
    written in accordance with properly reviewed and approved procedures; equipment was
*  
    returned to its operational status following testing (temporary modifications or jumpers
Repair of Unit 2 AFW flow control valve flow retention issue;  
    required for test performance were properly removed after test completion); and test
*  
    documentation was properly evaluated. The inspectors evaluated the activities against
Repair of circuitry associated with failure of fast transfer and generator trip during  
    TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
dual-unit trip; and  
    NRC generic communications to ensure that the test results adequately ensured that the
*  
    equipment met the licensing basis and design requirements. In addition, the inspectors
Unit 1 TDAFW repairs following inadvertent trip.  
    reviewed corrective action documents associated with post-maintenance tests to
These activities were selected based upon the structure, system, or component's ability  
    determine whether the licensee was identifying problems and entering them in the CAP
to impact risk. The inspectors evaluated these activities for the following (as applicable):  
    and that the problems were being corrected commensurate with their importance to
the effect of testing on the plant had been adequately addressed; testing was adequate  
    safety. Documents reviewed are listed in the Attachment to this report.
for the maintenance performed; acceptance criteria were clear and demonstrated  
    This inspection constituted eight post-maintenance testing samples as defined in
operational readiness; test instrumentation was appropriate; tests were performed as  
    IP 71111.19-05.
written in accordance with properly reviewed and approved procedures; equipment was  
                                              24
returned to its operational status following testing (temporary modifications or jumpers  
required for test performance were properly removed after test completion); and test  
documentation was properly evaluated. The inspectors evaluated the activities against  
TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various  
NRC generic communications to ensure that the test results adequately ensured that the  
equipment met the licensing basis and design requirements. In addition, the inspectors  
reviewed corrective action documents associated with post-maintenance tests to  
determine whether the licensee was identifying problems and entering them in the CAP  
and that the problems were being corrected commensurate with their importance to  
safety. Documents reviewed are listed in the Attachment to this report.  
This inspection constituted eight post-maintenance testing samples as defined in  
IP 71111.19-05.  


b. Findings
  Introduction: A finding of very low safety significance (Green) with an associated NCV of
25
  TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1 TDAFW
  pump tripped during an emergent dual-unit shutdown. Both units were taken offline by
b.  
  operators due to debris intrusion from Lake Michigan into the cooling water
Findings  
  screenhouse. The TDAFW pump started as expected but shutdown after a few minutes
Introduction: A finding of very low safety significance (Green) with an associated NCV of  
  of operation.
TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1 TDAFW  
  Description: On November 1, 2014, operators removed both units from service in
pump tripped during an emergent dual-unit shutdown. Both units were taken offline by  
  response to excessive debris intrusion into the cooling water screenhouse. Following
operators due to debris intrusion from Lake Michigan into the cooling water  
  the trip of both reactors, AFW pumps started as expected. However, the Unit 1 TDAFW
screenhouse. The TDAFW pump started as expected but shutdown after a few minutes  
  unexpectedly turned off after a few minutes of operation while operators were adjusting
of operation.
  flow to the steam generators. Adequate flow continued to be provided by the two other
Description: On November 1, 2014, operators removed both units from service in  
  AFW pumps. During the ensuing forced outage to address the debris intrusion issue,
response to excessive debris intrusion into the cooling water screenhouse. Following  
  the licensee performed an investigation into why the pump tripped off. The licensee
the trip of both reactors, AFW pumps started as expected. However, the Unit 1 TDAFW  
  explored and ruled out causes such as a pump overspeed, failed overspeed trip circuitry,
unexpectedly turned off after a few minutes of operation while operators were adjusting  
  and governor control problems. The investigation included several test runs of the pump
flow to the steam generators. Adequate flow continued to be provided by the two other  
  while rapidly changing demand in an effort to stress the pump and replicate the trip
AFW pumps. During the ensuing forced outage to address the debris intrusion issue,  
  event. During continued troubleshooting, the licensee later discovered a protective
the licensee performed an investigation into why the pump tripped off. The licensee  
  enclosure around an electronic component (the trip solenoid) had been installed
explored and ruled out causes such as a pump overspeed, failed overspeed trip circuitry,  
  incorrectly. The enclosure was relatively loose, and the licensee found by moving it
and governor control problems. The investigation included several test runs of the pump  
  slightly, it could be placed in a position where a threaded rod on the enclosure could
while rapidly changing demand in an effort to stress the pump and replicate the trip  
  interfere with the proper latching of the TTV for the pump. When the pump turns on, the
event. During continued troubleshooting, the licensee later discovered a protective  
  TTV opens to admit steam to the turbine. As the valve stem moves up, an attachment
enclosure around an electronic component (the trip solenoid) had been installed  
  engages a trip hook. The trip hook basically acts to hold the valve open. On a trip
incorrectly. The enclosure was relatively loose, and the licensee found by moving it  
  condition, such as a pump overspeed, the hook would move out of the way, allowing the
slightly, it could be placed in a position where a threaded rod on the enclosure could  
  valve to shut and the pump to turn off. Precise engagement between the TTV and the
interfere with the proper latching of the TTV for the pump. When the pump turns on, the  
  trip hook is required for the pump to operate correctly. In this case, the licensees
TTV opens to admit steam to the turbine. As the valve stem moves up, an attachment  
  apparent cause evaluation determined the most likely cause was inadequate trip hook
engages a trip hook. The trip hook basically acts to hold the valve open. On a trip  
  engagement as a result of the interference from the trip solenoid enclosure. As part of
condition, such as a pump overspeed, the hook would move out of the way, allowing the  
  the extent-of-condition, the licensee discovered the same potential issue on the Unit 2
valve to shut and the pump to turn off. Precise engagement between the TTV and the  
  TDAFW pump. Further investigation revealed that the enclosure was not captured in
trip hook is required for the pump to operate correctly. In this case, the licensees  
  design diagrams, and that work instructions regarding its installation/removal were not
apparent cause evaluation determined the most likely cause was inadequate trip hook  
  detailed. Most recently, the Unit 1 TDAFW pump trip solenoid enclosure had been
engagement as a result of the interference from the trip solenoid enclosure. As part of  
  removed and reinstalled during the Fall 2014 refueling outage as part of planned
the extent-of-condition, the licensee discovered the same potential issue on the Unit 2  
  maintenance. Working with the pump vendor, the licensee identified the correct
TDAFW pump. Further investigation revealed that the enclosure was not captured in  
  configuration of the enclosure and reinstalled them correctly on both pumps. The
design diagrams, and that work instructions regarding its installation/removal were not  
  licensee tested the pump several times afterwards, and restored the Unit 1 TDAFW
detailed. Most recently, the Unit 1 TDAFW pump trip solenoid enclosure had been  
  pump to operable status at the conclusion of the forced outage.
removed and reinstalled during the Fall 2014 refueling outage as part of planned  
  Analysis: The failure to have adequate instructions for performing work on safety-related
maintenance. Working with the pump vendor, the licensee identified the correct  
  equipment, as required by TS 5.4, Procedures, was a performance deficiency
configuration of the enclosure and reinstalled them correctly on both pumps. The  
  warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued
licensee tested the pump several times afterwards, and restored the Unit 1 TDAFW  
  September 7, 2012. The performance deficiency was more than minor because it
pump to operable status at the conclusion of the forced outage.  
  adversely impacted the Configuration Control attribute of the Mitigating Systems
Analysis: The failure to have adequate instructions for performing work on safety-related  
  cornerstone, whose objective is ensuring the availability, reliability, and capability of
equipment, as required by TS 5.4, Procedures, was a performance deficiency  
  systems that respond to initiating events to prevent undesirable consequences.
warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued  
  The inspectors utilized IMC 0609 Appendix A, The Significance Determination Process
September 7, 2012. The performance deficiency was more than minor because it  
  for Findings at Power, issued June 19, 2012, to assess the significance of the finding.
adversely impacted the Configuration Control attribute of the Mitigating Systems  
                                              25
cornerstone, whose objective is ensuring the availability, reliability, and capability of  
systems that respond to initiating events to prevent undesirable consequences.  
The inspectors utilized IMC 0609 Appendix A, The Significance Determination Process  
for Findings at Power, issued June 19, 2012, to assess the significance of the finding.


Per Exhibit 2, the finding represented a loss of function for one train of AFW for greater
than the TS allowed outage time. Therefore, the inspectors consulted the regional
26
Senior Reactor Analyst (SRA) for a detailed risk evaluation. The inspectors considered
the Unit 1 TDAFW pump inoperable since the last successful surveillance on
Per Exhibit 2, the finding represented a loss of function for one train of AFW for greater  
October 23. Given the evidence available, this was the likely opportunity for the
than the TS allowed outage time. Therefore, the inspectors consulted the regional  
conditions to be established to set-up the improper engagement between the TTV and
Senior Reactor Analyst (SRA) for a detailed risk evaluation. The inspectors considered  
the trip hook.
the Unit 1 TDAFW pump inoperable since the last successful surveillance on
The Region III SRA used the NRC standardized plant analysis risk model for D.C. Cook
October 23. Given the evidence available, this was the likely opportunity for the  
to perform a detailed risk evaluation. The model has internal and external event
conditions to be established to set-up the improper engagement between the TTV and  
initiators. The SRA assumed an exposure period for the condition of 9 days. The delta
the trip hook.  
core damage frequency (CDF) calculated was 4.5E-7/yr, which is a finding of very low
The Region III SRA used the NRC standardized plant analysis risk model for D.C. Cook  
safety significance (Green). The dominant risk sequence was a fire in the turbine
to perform a detailed risk evaluation. The model has internal and external event  
building, followed by a failure of main feedwater, auxiliary feedwater and feed and bleed.
initiators. The SRA assumed an exposure period for the condition of 9 days. The delta  
Since the calculated delta CDF was greater than 1E-7/yr, the SRA also considered the
core damage frequency (CDF) calculated was 4.5E-7/yr, which is a finding of very low  
potential impact of the finding on large early release frequency using IMC 0609
safety significance (Green). The dominant risk sequence was a fire in the turbine  
Appendix H, Containment Integrity Significance Determination Process. The plant has
building, followed by a failure of main feedwater, auxiliary feedwater and feed and bleed.
an ice condenser containment and sequences important to large early release frequency
Since the calculated delta CDF was greater than 1E-7/yr, the SRA also considered the  
are steam generator tube rupture, inter-system loss-of-coolant accident, and station
potential impact of the finding on large early release frequency using IMC 0609  
blackout. Some of the sequences that contributed to the change in CDF included station
Appendix H, Containment Integrity Significance Determination Process. The plant has  
blackout sequences but their contribution was less than 1E-7/yr. The SRA concluded
an ice condenser containment and sequences important to large early release frequency  
that the risk of this finding should be characterized by the overall change in CDF.
are steam generator tube rupture, inter-system loss-of-coolant accident, and station  
The finding had an associated cross-cutting aspect in the area of human performance,
blackout. Some of the sequences that contributed to the change in CDF included station  
specifically, H.8, Procedure Adherence. Safety Culture Common Language Initiative
blackout sequences but their contribution was less than 1E-7/yr. The SRA concluded  
NUREG-2165 provides an example of the aspect as individuals review procedures
that the risk of this finding should be characterized by the overall change in CDF.  
before work to validate they are appropriate for scope of work, and ensure required
The finding had an associated cross-cutting aspect in the area of human performance,  
changes are completed before implementation. Contrary to this description, work
specifically, H.8, Procedure Adherence. Safety Culture Common Language Initiative  
proceeded on the trip enclosure despite a lack of detailed instructions on the
NUREG-2165 provides an example of the aspect as individuals review procedures  
removal/installation of the enclosure.
before work to validate they are appropriate for scope of work, and ensure required  
Enforcement: Technical Specification 5.4, Procedures, states, in part, that written
changes are completed before implementation. Contrary to this description, work  
procedures shall be established, implemented, and maintained covering the applicable
proceeded on the trip enclosure despite a lack of detailed instructions on the  
procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in
removal/installation of the enclosure.  
part, that maintenance that can affect the performance of safety-related equipment
Enforcement: Technical Specification 5.4, Procedures, states, in part, that written  
should be properly preplanned and performed in accordance with written procedures,
procedures shall be established, implemented, and maintained covering the applicable  
documented instructions, or drawings appropriate to the circumstances.
procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in  
Contrary to those requirements, work was performed on the Unit 1 TDAFW pump trip
part, that maintenance that can affect the performance of safety-related equipment  
solenoid enclosure with inadequate work instructions. As a result, an apparent cause
should be properly preplanned and performed in accordance with written procedures,  
evaluation determined the misplaced enclosure was the likely cause of the pump
documented instructions, or drawings appropriate to the circumstances.  
failure during an actual demand following a dual-unit trip. The violation existed from
Contrary to those requirements, work was performed on the Unit 1 TDAFW pump trip  
October 23, 2014, until troubleshooting and post-maintenance testing activities were
solenoid enclosure with inadequate work instructions. As a result, an apparent cause  
completed on November 3, 2014, following the dual-unit trip.
evaluation determined the misplaced enclosure was the likely cause of the pump
For immediate corrective actions, the licensee initiated AR-2014-13668 and began
failure during an actual demand following a dual-unit trip. The violation existed from  
troubleshooting activities. The licensee investigation revealed the misplaced trip
October 23, 2014, until troubleshooting and post-maintenance testing activities were  
solenoid enclosure to be the likely cause of the pump trip. Subsequently, the enclosures
completed on November 3, 2014, following the dual-unit trip.  
were installed in the correct position. This violation is being treated as an NCV,
For immediate corrective actions, the licensee initiated AR-2014-13668 and began  
consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety
troubleshooting activities. The licensee investigation revealed the misplaced trip  
                                          26
solenoid enclosure to be the likely cause of the pump trip. Subsequently, the enclosures  
were installed in the correct position. This violation is being treated as an NCV,  
consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety  


      significance and was entered into the licensees CAP. (NCV 05000315/2014005-04;
      Inadvertent Trip of the Unit 1 TDAFW Pump)
27
1R20 Outage Activities (71111.20)
.1   Refueling Outage Activities
significance and was entered into the licensees CAP. (NCV 05000315/2014005-04;  
  a. Inspection Scope
Inadvertent Trip of the Unit 1 TDAFW Pump)  
      The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 1
1R20 Outage Activities (71111.20)  
      refueling outage, conducted September 24 - October 24, 2014, to confirm that the
.1  
      licensee had appropriately considered risk, industry experience, and previous
Refueling Outage Activities  
      site-specific problems in developing and implementing a plan that assured maintenance
a.  
      of defense-in-depth. During the refueling outage, the inspectors observed portions of
Inspection Scope  
      the shutdown and cooldown processes and monitored licensee controls over the outage
The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 1  
      activities listed below:
refueling outage, conducted September 24 - October 24, 2014, to confirm that the  
      *       licensee configuration management, including maintenance of defense-in-depth
licensee had appropriately considered risk, industry experience, and previous  
              commensurate with the Outage Safety Plan for key safety functions and
site-specific problems in developing and implementing a plan that assured maintenance  
              compliance with the applicable TS when taking equipment out of service;
of defense-in-depth. During the refueling outage, the inspectors observed portions of  
      *       implementation of clearance activities and confirmation that tags were properly
the shutdown and cooldown processes and monitored licensee controls over the outage  
              hung and equipment appropriately configured to safely support the work or
activities listed below:  
              testing;
*  
      *       installation and configuration of reactor coolant pressure, level, and temperature
licensee configuration management, including maintenance of defense-in-depth  
              instruments to provide accurate indication, accounting for instrument error;
commensurate with the Outage Safety Plan for key safety functions and  
      *       controls over the status and configuration of electrical systems to ensure that
compliance with the applicable TS when taking equipment out of service;  
              TS and Outage Safety Plan requirements were met, and controls over switchyard
*  
              activities;
implementation of clearance activities and confirmation that tags were properly  
      *       monitoring of decay heat removal processes, systems, and components;
hung and equipment appropriately configured to safely support the work or  
      *       controls to ensure that outage work was not impacting the ability of the operators
testing;  
              to operate the spent fuel pool cooling system;
*  
      *       reactor water inventory controls including flow paths, configurations, and
installation and configuration of reactor coolant pressure, level, and temperature  
              alternative means for inventory addition, and controls to prevent inventory loss;
instruments to provide accurate indication, accounting for instrument error;  
      *       controls over activities that could affect reactivity;
*  
      *       maintenance of secondary containment as required by TS;
controls over the status and configuration of electrical systems to ensure that  
      *       licensee fatigue management, as required by 10 CFR 26, Subpart I;
TS and Outage Safety Plan requirements were met, and controls over switchyard  
      *       refueling activities, including fuel handling and sipping to detect fuel assembly
activities;  
              leakage;
*  
      *       startup and ascension to full power operation, tracking of startup prerequisites,
monitoring of decay heat removal processes, systems, and components;  
              walkdown of the drywell (primary containment) to verify that debris had not been
*  
              left which could block emergency core cooling system suction strainers, and
controls to ensure that outage work was not impacting the ability of the operators  
              reactor physics testing; and
to operate the spent fuel pool cooling system;  
      *       licensee identification and resolution of problems related to refueling outage
*  
              activities.
reactor water inventory controls including flow paths, configurations, and  
      Documents reviewed are listed in the Attachment to this report.
alternative means for inventory addition, and controls to prevent inventory loss;  
      This inspection constituted one Refueling Outage sample as defined in IP 71111.20-05.
*  
                                                  27
controls over activities that could affect reactivity;  
*  
maintenance of secondary containment as required by TS;  
*  
licensee fatigue management, as required by 10 CFR 26, Subpart I;  
*  
refueling activities, including fuel handling and sipping to detect fuel assembly  
leakage;  
*  
startup and ascension to full power operation, tracking of startup prerequisites,  
walkdown of the drywell (primary containment) to verify that debris had not been  
left which could block emergency core cooling system suction strainers, and  
reactor physics testing; and  
*  
licensee identification and resolution of problems related to refueling outage  
activities.  
Documents reviewed are listed in the Attachment to this report.  
This inspection constituted one Refueling Outage sample as defined in IP 71111.20-05.  


  b. Findings
      No findings were identified.
28
.2   Unit 1 and Unit 2 Forced Outages Commencing November 1, 2014
  a. Inspection Scope
b.  
      On November 1, rough lake conditions generated substantial amounts of debris that
Findings  
      clogged trash racks and travelling screens. The licensee manually tripped the Unit 1
No findings were identified.  
      reactor and initially reduced power to 50 percent on the Unit 2 reactor to reduce
.2  
      circulating water flow. Conditions continued to degrade; therefore the licensee
Unit 1 and Unit 2 Forced Outages Commencing November 1, 2014  
      subsequently tripped the Unit 2 reactor. Unit 1 remained in Mode 3 and returned to
a.  
      100 percent power on November 8. Unit 2 was cooled down to Mode 5 to repair an
Inspection Scope  
      intermediate range nuclear instrument. Unit 2 was returned to 100 percent power on
On November 1, rough lake conditions generated substantial amounts of debris that  
      November 13. The inspectors toured portions of containment, observed shutdown and
clogged trash racks and travelling screens. The licensee manually tripped the Unit 1  
      startup activities, assessed plant risk, and observed maintenance activities.
reactor and initially reduced power to 50 percent on the Unit 2 reactor to reduce  
      This inspection constituted one Forced Outage sample as defined in IP 71111.20-05.
circulating water flow. Conditions continued to degrade; therefore the licensee  
  b. Findings
subsequently tripped the Unit 2 reactor. Unit 1 remained in Mode 3 and returned to
      No findings were identified.
100 percent power on November 8. Unit 2 was cooled down to Mode 5 to repair an  
1R22 Surveillance Testing (71111.22)
intermediate range nuclear instrument. Unit 2 was returned to 100 percent power on  
  a. Inspection Scope
November 13. The inspectors toured portions of containment, observed shutdown and  
      The inspectors reviewed the test results for the following activities to determine whether
startup activities, assessed plant risk, and observed maintenance activities.  
      risk-significant systems and equipment were capable of performing their intended safety
This inspection constituted one Forced Outage sample as defined in IP 71111.20-05.  
      function and to verify testing was conducted in accordance with applicable procedural
b.  
      and TS requirements:
Findings  
      *       1-OHP-4030-108-008R, Unit 1 ECCS Check Valve Test, (IST);
No findings were identified.  
      *       1-EHP-4030-134-203, Unit 1 LLRT (Containment Isolation Valve);
1R22 Surveillance Testing (71111.22)  
      *       12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance,
a.  
              (Ice Condenser Surveillance);
Inspection Scope  
      *       Unit 1 Control Room Emergency Ventilation Surveillance, 1-EHP-4030-128-229
The inspectors reviewed the test results for the following activities to determine whether  
              (Routine); and
risk-significant systems and equipment were capable of performing their intended safety  
      *       Loss of Offsite Power/Loss-of-Coolant Accident Circuit Testing (Routine).
function and to verify testing was conducted in accordance with applicable procedural  
      The inspectors observed in-plant activities and reviewed procedures and associated
and TS requirements:  
      records to determine the following:
*  
      *       did preconditioning occur;
1-OHP-4030-108-008R, Unit 1 ECCS Check Valve Test, (IST);  
      *       the effects of the testing were adequately addressed by control room personnel
*  
              or engineers prior to the commencement of the testing;
1-EHP-4030-134-203, Unit 1 LLRT (Containment Isolation Valve);  
      *       acceptance criteria were clearly stated, demonstrated operational readiness, and
*  
              were consistent with the system design basis;
12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance,
      *       plant equipment calibration was correct, accurate, and properly documented;
(Ice Condenser Surveillance);  
      *       as-left setpoints were within required ranges; and the calibration frequency was
*  
              in accordance with TSs, the USAR, procedures, and applicable commitments;
Unit 1 Control Room Emergency Ventilation Surveillance, 1-EHP-4030-128-229  
                                                28
(Routine); and  
*  
Loss of Offsite Power/Loss-of-Coolant Accident Circuit Testing (Routine).  
The inspectors observed in-plant activities and reviewed procedures and associated  
records to determine the following:  
*  
did preconditioning occur;
*  
the effects of the testing were adequately addressed by control room personnel  
or engineers prior to the commencement of the testing;  
*  
acceptance criteria were clearly stated, demonstrated operational readiness, and  
were consistent with the system design basis;  
*  
plant equipment calibration was correct, accurate, and properly documented;  
*  
as-left setpoints were within required ranges; and the calibration frequency was  
in accordance with TSs, the USAR, procedures, and applicable commitments;  


    *       measuring and test equipment calibration was current;
    *       test equipment was used within the required range and accuracy; applicable
29
            prerequisites described in the test procedures were satisfied;
    *       test frequencies met TS requirements to demonstrate operability and reliability;
*  
            tests were performed in accordance with the test procedures and other
measuring and test equipment calibration was current;  
            applicable procedures; jumpers and lifted leads were controlled and restored
*  
            where used;
test equipment was used within the required range and accuracy; applicable  
    *       test data and results were accurate, complete, within limits, and valid;
prerequisites described in the test procedures were satisfied;  
    *       test equipment was removed after testing;
*  
    *       where applicable for inservice testing activities, testing was performed in
test frequencies met TS requirements to demonstrate operability and reliability;  
            accordance with the applicable version of Section XI, American Society of
tests were performed in accordance with the test procedures and other  
            Mechanical Engineers code, and reference values were consistent with the
applicable procedures; jumpers and lifted leads were controlled and restored  
            system design basis;
where used;  
    *       where applicable, test results not meeting acceptance criteria were addressed
*  
            with an adequate operability evaluation or the system or component was
test data and results were accurate, complete, within limits, and valid;  
            declared inoperable;
*  
    *       where applicable for safety-related instrument control surveillance tests,
test equipment was removed after testing;  
            reference setting data were accurately incorporated in the test procedure;
*  
    *       where applicable, actual conditions encountering high resistance electrical
where applicable for inservice testing activities, testing was performed in  
            contacts were such that the intended safety function could still be accomplished;
accordance with the applicable version of Section XI, American Society of  
    *       prior procedure changes had not provided an opportunity to identify problems
Mechanical Engineers code, and reference values were consistent with the  
            encountered during the performance of the surveillance or calibration test;
system design basis;  
    *       equipment was returned to a position or status required to support the
*  
            performance of its safety functions; and
where applicable, test results not meeting acceptance criteria were addressed  
    *       all problems identified during the testing were appropriately documented and
with an adequate operability evaluation or the system or component was  
            dispositioned in the CAP.
declared inoperable;  
    Documents reviewed are listed in the Attachment to this report.
*  
    This inspection constituted two routine surveillance testing samples, one inservice
where applicable for safety-related instrument control surveillance tests,  
    testing sample, one ice condenser surveillance, and one containment isolation valve
reference setting data were accurately incorporated in the test procedure;  
    sample as defined in IP 71111.22, Sections-02 and-05.
*  
  b. Findings
where applicable, actual conditions encountering high resistance electrical  
    No findings were identified.
contacts were such that the intended safety function could still be accomplished;  
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
*  
  a. Inspection Scope
prior procedure changes had not provided an opportunity to identify problems  
    The regional inspectors performed an in-office review of the latest revisions to the
encountered during the performance of the surveillance or calibration test;  
    Emergency Plan and Emergency Plan Implementing Procedures as listed in the
*  
    Attachment to this report.
equipment was returned to a position or status required to support the  
    The licensee transmitted the Emergency Plan and Emergency Action Level revisions to
performance of its safety functions; and  
    the NRC pursuant to the requirements of 10 CFR Part 50, Appendix E, Section V,
*  
    Implementing Procedures. The NRC review was not documented in a safety
all problems identified during the testing were appropriately documented and  
    evaluation report and did not constitute approval of licensee-generated changes;
dispositioned in the CAP.  
    therefore, this revision is subject to future inspection. The specific documents reviewed
Documents reviewed are listed in the Attachment to this report.  
    during this inspection are listed in the Attachment to this report.
This inspection constituted two routine surveillance testing samples, one inservice  
                                                29
testing sample, one ice condenser surveillance, and one containment isolation valve  
sample as defined in IP 71111.22, Sections-02 and-05.  
b.  
Findings  
No findings were identified.  
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)  
a.  
Inspection Scope  
The regional inspectors performed an in-office review of the latest revisions to the  
Emergency Plan and Emergency Plan Implementing Procedures as listed in the  
Attachment to this report.  
The licensee transmitted the Emergency Plan and Emergency Action Level revisions to  
the NRC pursuant to the requirements of 10 CFR Part 50, Appendix E, Section V,  
Implementing Procedures. The NRC review was not documented in a safety  
evaluation report and did not constitute approval of licensee-generated changes;  
therefore, this revision is subject to future inspection. The specific documents reviewed  
during this inspection are listed in the Attachment to this report.


  This Emergency Action Level and Emergency Plan Change inspection constituted one
  sample as defined in IP 71114.04-06.
30
b. Findings
  Introduction: An Unresolved Item (URI) was identified because additional information is
This Emergency Action Level and Emergency Plan Change inspection constituted one  
  required to determine whether a performance deficiency that is more than minor exists
sample as defined in IP 71114.04-06.  
  and if a violation of 10 CFR 50.54(q)(3) occurred. The inspectors identified an issue of
b.  
  concern for a change to the Donald C. Cook Emergency Plan, Table 1, that reduced the
Findings  
  number of Radiation Protection Technicians (RPTs) required to augment the on-shift
Introduction: An Unresolved Item (URI) was identified because additional information is  
  emergency response organization in 60 minutes of a declared emergency and replaced
required to determine whether a performance deficiency that is more than minor exists  
  them with a Radiological Assessment Coordinator (RAC) and an Environmental
and if a violation of 10 CFR 50.54(q)(3) occurred. The inspectors identified an issue of  
  Assessment Coordinator (EAC).
concern for a change to the Donald C. Cook Emergency Plan, Table 1, that reduced the  
  Description. During the review, the inspectors identified a change made in Table 1 of
number of Radiation Protection Technicians (RPTs) required to augment the on-shift  
  Revision 35 to the Emergency-Plan (E-Plan), dated June 3, 2014. The change reduced
emergency response organization in 60 minutes of a declared emergency and replaced  
  the number of 60-minute response RPTs tasked with conducting offsite surveys from
them with a Radiological Assessment Coordinator (RAC) and an Environmental  
  three RPTs to two RPTs and one EAC. The second change reduced the number of
Assessment Coordinator (EAC).
  60-minute response RPTs tasked with conducting in-plant surveys from two RPTs to one
Description. During the review, the inspectors identified a change made in Table 1 of  
  RPT and one RAC. According the licensees 10 CFR 2014 50.54(q) screening
Revision 35 to the Emergency-Plan (E-Plan), dated June 3, 2014. The change reduced  
  evaluation, this change was to align the wording in Table 1 with Sections B.5.a.4 and
the number of 60-minute response RPTs tasked with conducting offsite surveys from  
  B.5.c.4 of the E-Plan. The inspectors identified that the wording in Section B.5.a.4 and
three RPTs to two RPTs and one EAC. The second change reduced the number of  
  B.5.c.4 of the E-Plan had been changed to include the EAC and the RAC as 60-minute
60-minute response RPTs tasked with conducting in-plant surveys from two RPTs to one  
  responders in Revision 19 of the plan in March of 2004. Inspectors review of the
RPT and one RAC. According the licensees 10 CFR 2014 50.54(q) screening  
  10 CFR 50.54(q) screening for the changes in Revision 19, identified no evaluations had
evaluation, this change was to align the wording in Table 1 with Sections B.5.a.4 and  
  been done for this change. The inspectors reviewed Revision 18 of the E-Plan and the
B.5.c.4 of the E-Plan. The inspectors identified that the wording in Section B.5.a.4 and  
  associated March 21, 2003 licensee request for prior approval for changes to the E-plan
B.5.c.4 of the E-Plan had been changed to include the EAC and the RAC as 60-minute  
  that was conducted, approved by the NRC, and implemented in this revision. The NRC
responders in Revision 19 of the plan in March of 2004. Inspectors review of the  
  approved change request included specific numbers of RPTs for 60-minute response
10 CFR 50.54(q) screening for the changes in Revision 19, identified no evaluations had  
  tasks of three RPTs for offsite surveys and 2 RPTs for onsite surveys.
been done for this change. The inspectors reviewed Revision 18 of the E-Plan and the  
  The licensee indicated that the EAC and RAC were not currently qualified RPTs. This
associated March 21, 2003 licensee request for prior approval for changes to the E-plan  
  suggests a performance deficiency, due to the appearance of a reduction in
that was conducted, approved by the NRC, and implemented in this revision. The NRC  
  effectiveness to the licensees E-plan, without prior NRC approval. However, in order to
approved change request included specific numbers of RPTs for 60-minute response  
  determine if this is a performance deficiency of more than minor significance, additional
tasks of three RPTs for offsite surveys and 2 RPTs for onsite surveys.  
  information is required to understand if the RAC and EAC positions had equivalent
The licensee indicated that the EAC and RAC were not currently qualified RPTs. This  
  capabilities as the qualified RPTs. The licensee has entered this issue in their
suggests a performance deficiency, due to the appearance of a reduction in  
  Corrective Action Program as AR 2014-15685, Potential EP Finding. Compensatory
effectiveness to the licensees E-plan, without prior NRC approval. However, in order to  
  actions were taken while their staff gathers additional information, which included
determine if this is a performance deficiency of more than minor significance, additional  
  requiring two additional qualified RPTs to respond to the Operations Support Center
information is required to understand if the RAC and EAC positions had equivalent  
  within 60 minutes prior to activating the facility in the event of a declared emergency.
capabilities as the qualified RPTs. The licensee has entered this issue in their  
  The licensee stated that it will provide the inspectors with additional information within
Corrective Action Program as AR 2014-15685, Potential EP Finding. Compensatory  
  30 days of the exit meeting.
actions were taken while their staff gathers additional information, which included  
  Therefore, a URI was identified pending additional information. Specifically,
requiring two additional qualified RPTs to respond to the Operations Support Center  
  documentation demonstrating the knowledge, skills, and abilities of the EAC and RAC
within 60 minutes prior to activating the facility in the event of a declared emergency.  
  are equivalent to the RPTs is necessary for the inspectors to determine whether the
The licensee stated that it will provide the inspectors with additional information within
  performance deficiency is more than minor and if a violation of 10 CFR 50.54(q)
30 days of the exit meeting.
  occurred. (URI 05000315/2014005-05; Changes to Minimum 60-Minute Emergency
Therefore, a URI was identified pending additional information. Specifically,  
  Responder Staffing Without Prior Approval)
documentation demonstrating the knowledge, skills, and abilities of the EAC and RAC  
                                            30
are equivalent to the RPTs is necessary for the inspectors to determine whether the  
performance deficiency is more than minor and if a violation of 10 CFR 50.54(q)  
occurred. (URI 05000315/2014005-05; Changes to Minimum 60-Minute Emergency  
Responder Staffing Without Prior Approval)


2.   RADIATION SAFETY
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
31
      The inspection activities supplement those documented in NRC Inspection Report
      05000315-05000316/2014002 and constitute one complete sample as defined in
2.  
      Inspection Procedure 71124.01-05.
RADIATION SAFETY  
.1   Radiological Hazard Assessment (02.02)
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)  
  a. Inspection Scope
The inspection activities supplement those documented in NRC Inspection Report  
      The inspectors determined whether there have been changes to plant operations since
05000315-05000316/2014002 and constitute one complete sample as defined in  
      the last inspection that may result in a significant new radiological hazard for onsite
Inspection Procedure 71124.01-05.  
      workers or members of the public. The inspectors evaluated whether the licensee
.1  
      assessed the potential impact of these changes and has implemented periodic
Radiological Hazard Assessment (02.02)
      monitoring, as appropriate, to detect and quantify the radiological hazard.
a.  
      The inspectors reviewed the last two radiological surveys from selected plant areas and
Inspection Scope  
      evaluated whether the thoroughness and frequency of the surveys where appropriate for
The inspectors determined whether there have been changes to plant operations since  
      the given radiological hazard.
the last inspection that may result in a significant new radiological hazard for onsite  
      The inspectors selected the following radiologically risk significant work activities that
workers or members of the public. The inspectors evaluated whether the licensee  
      involved exposure to radiation:
assessed the potential impact of these changes and has implemented periodic  
      *       Refuel Cavity Decontamination Activities;
monitoring, as appropriate, to detect and quantify the radiological hazard.  
      *       Steam Generator Platform Activities;
The inspectors reviewed the last two radiological surveys from selected plant areas and  
      *       Valve Maintenance / Repair;
evaluated whether the thoroughness and frequency of the surveys where appropriate for  
      *       Perform Radiography in Auxiliary and Turbine Buildings and Plant Restricted
the given radiological hazard.  
              Areas; and
The inspectors selected the following radiologically risk significant work activities that  
      *       Reactor Pit Very High Radiation Area (VHRA) Downpost Survey.
involved exposure to radiation:  
      For these work activities, the inspectors assessed whether the pre-work surveys
*  
      performed were appropriate to identify and quantify the radiological hazard and to
Refuel Cavity Decontamination Activities;
      establish adequate protective measures. The inspectors evaluated the radiological
*  
      survey program to determine if hazards were properly identified, including the following:
Steam Generator Platform Activities;
      *       identification of hot particles;
*  
      *       the presence of alpha emitters;
Valve Maintenance / Repair;
      *       the potential for airborne radioactive materials, including the potential presence
*  
              of transuranics and/or other hard-to-detect radioactive materials (This evaluation
Perform Radiography in Auxiliary and Turbine Buildings and Plant Restricted  
              may include licensee planned entry into non-routinely entered areas subject to
Areas; and  
              previous contamination from failed fuel.);
*  
      *       the hazards associated with work activities that could suddenly and severely
Reactor Pit Very High Radiation Area (VHRA) Downpost Survey.  
              increase radiological conditions and that the licensee has established a means to
For these work activities, the inspectors assessed whether the pre-work surveys  
              inform workers of changes that could significantly impact their occupational dose;
performed were appropriate to identify and quantify the radiological hazard and to  
              and
establish adequate protective measures. The inspectors evaluated the radiological  
      *       severe radiation field dose gradients that can result in non-uniform exposures of
survey program to determine if hazards were properly identified, including the following:
              the body.
*  
                                                31
identification of hot particles;  
*  
the presence of alpha emitters;  
*  
the potential for airborne radioactive materials, including the potential presence  
of transuranics and/or other hard-to-detect radioactive materials (This evaluation  
may include licensee planned entry into non-routinely entered areas subject to  
previous contamination from failed fuel.);
*  
the hazards associated with work activities that could suddenly and severely  
increase radiological conditions and that the licensee has established a means to  
inform workers of changes that could significantly impact their occupational dose;  
and  
*  
severe radiation field dose gradients that can result in non-uniform exposures of  
the body.  


    The inspectors observed work in potential airborne areas and evaluated whether the air
    samples were representative of the breathing air zone. The inspectors evaluated
32
    whether continuous air monitors were located in areas with low background to minimize
    false alarms and were representative of actual work areas. The inspectors evaluated
The inspectors observed work in potential airborne areas and evaluated whether the air  
    the licensees program for monitoring levels of loose surface contamination in areas of
samples were representative of the breathing air zone. The inspectors evaluated  
    the plant with the potential for the contamination to become airborne.
whether continuous air monitors were located in areas with low background to minimize  
  b. Findings
false alarms and were representative of actual work areas. The inspectors evaluated  
    No findings were identified.
the licensees program for monitoring levels of loose surface contamination in areas of  
.2   Instructions to Workers (02.03)
the plant with the potential for the contamination to become airborne.  
  a. Inspection Scope
b.  
    The inspectors reviewed the following radiation work permits used to access high
Findings  
    radiation areas and evaluated the specified work control instructions or control barriers:
No findings were identified.  
    *       RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
.2  
    *       RWP 141148; U1C26 - Steam Generator Platform Activities;
Instructions to Workers (02.03)  
    *       RWP 141145; U1C26 - Valve Maintenance / Repair;
a.  
    *       RWP 1 41130; U1C26 - Perform Radiography in Auxiliary & Turbine Buildings &
Inspection Scope  
            Plant Restricted Areas; and
The inspectors reviewed the following radiation work permits used to access high  
    *       RWP 141172; U1C26 - Reactor Pit VHRA Downpost Survey.
radiation areas and evaluated the specified work control instructions or control barriers:  
    For these radiation work permits, the inspectors assessed whether allowable stay times
*  
    or permissible dose (including from the intake of radioactive material) for radiologically
RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
    significant work under each radiation work permit were clearly identified. The inspectors
*  
    evaluated whether electronic personal dosimeter alarm set-points were in conformance
RWP 141148; U1C26 - Steam Generator Platform Activities;
    with survey indications and plant policy.
*  
    For work activities that could suddenly and severely increase radiological conditions, the
RWP 141145; U1C26 - Valve Maintenance / Repair;
    inspectors assessed the licensees means to inform workers of changes that could
*  
    significantly impact their occupational dose.
RWP 1 41130; U1C26 - Perform Radiography in Auxiliary & Turbine Buildings &  
  b. Findings
Plant Restricted Areas; and  
    No findings were identified.
*  
.3   Contamination and Radioactive Material Control (02.04)
RWP 141172; U1C26 - Reactor Pit VHRA Downpost Survey.  
  a. Inspection Scope
For these radiation work permits, the inspectors assessed whether allowable stay times  
    The inspectors observed locations where the licensee monitors potentially contaminated
or permissible dose (including from the intake of radioactive material) for radiologically  
    material leaving the radiological control area and inspected the methods used for
significant work under each radiation work permit were clearly identified. The inspectors  
    control, survey, and release from these areas. The inspectors observed the
evaluated whether electronic personal dosimeter alarm set-points were in conformance  
    performance of personnel surveying and releasing material for unrestricted use and
with survey indications and plant policy.  
    evaluated whether the work was performed in accordance with plant procedures and
For work activities that could suddenly and severely increase radiological conditions, the  
    whether the procedures were sufficient to control the spread of contamination and
inspectors assessed the licensees means to inform workers of changes that could  
    prevent unintended release of radioactive materials from the site. The inspectors
significantly impact their occupational dose.  
    assessed whether the radiation monitoring instrumentation had appropriate sensitivity for
b.  
    the type(s) of radiation present.
Findings  
                                              32
No findings were identified.  
.3  
Contamination and Radioactive Material Control (02.04)  
a.  
Inspection Scope  
The inspectors observed locations where the licensee monitors potentially contaminated  
material leaving the radiological control area and inspected the methods used for  
control, survey, and release from these areas. The inspectors observed the  
performance of personnel surveying and releasing material for unrestricted use and  
evaluated whether the work was performed in accordance with plant procedures and  
whether the procedures were sufficient to control the spread of contamination and  
prevent unintended release of radioactive materials from the site. The inspectors  
assessed whether the radiation monitoring instrumentation had appropriate sensitivity for  
the type(s) of radiation present.  


    The inspectors reviewed the licensees criteria for the survey and release of potentially
    contaminated material. The inspectors evaluated whether there was guidance on how to
33
    respond to an alarm that indicates the presence of licensed radioactive material.
    The inspectors reviewed the licensees procedures and records to verify that the
The inspectors reviewed the licensees criteria for the survey and release of potentially  
    radiation detection instrumentation was used at its typical sensitivity level based on
contaminated material. The inspectors evaluated whether there was guidance on how to  
    appropriate counting parameters. The inspectors assessed whether or not the licensee
respond to an alarm that indicates the presence of licensed radioactive material.  
    has established a de facto release limit by altering the instruments typical sensitivity
The inspectors reviewed the licensees procedures and records to verify that the  
    through such methods as raising the energy discriminator level or locating the instrument
radiation detection instrumentation was used at its typical sensitivity level based on  
    in a high-radiation background area.
appropriate counting parameters. The inspectors assessed whether or not the licensee  
    The inspectors selected several sealed sources from the licensees inventory records
has established a de facto release limit by altering the instruments typical sensitivity  
    and assessed whether the sources were accounted for and verified to be intact.
through such methods as raising the energy discriminator level or locating the instrument  
    The inspectors evaluated whether any transactions, since the last inspection, involving
in a high-radiation background area.  
    nationally tracked sources were reported in accordance with 10 CFR 20.2207.
The inspectors selected several sealed sources from the licensees inventory records  
  b. Findings
and assessed whether the sources were accounted for and verified to be intact.  
    No findings were identified.
The inspectors evaluated whether any transactions, since the last inspection, involving  
.4   Radiological Hazards Control and Work Coverage (02.05)
nationally tracked sources were reported in accordance with 10 CFR 20.2207.  
  a. Inspection Scope
b.  
    The inspectors evaluated ambient radiological conditions (e.g., radiation levels or
Findings  
    potential radiation levels) during tours of the facility. The inspectors assessed whether
No findings were identified.  
    the conditions were consistent with applicable posted surveys, radiation work permits,
.4  
    and worker briefings.
Radiological Hazards Control and Work Coverage (02.05)  
    The inspectors evaluated the adequacy of radiological controls, such as required
a.  
    surveys, radiation protection job coverage (including audio and visual surveillance for
Inspection Scope  
    remote job coverage), and contamination controls. The inspectors evaluated the
The inspectors evaluated ambient radiological conditions (e.g., radiation levels or  
    licensees use of electronic personal dosimeters in high noise areas as high radiation
potential radiation levels) during tours of the facility. The inspectors assessed whether  
    area monitoring devices.
the conditions were consistent with applicable posted surveys, radiation work permits,  
    The inspectors reviewed the application of dosimetry to effectively monitor exposure to
and worker briefings.  
    personnel in high-radiation work areas with significant dose rate gradients.
The inspectors evaluated the adequacy of radiological controls, such as required  
    The inspectors reviewed the following radiation work permits for work within airborne
surveys, radiation protection job coverage (including audio and visual surveillance for  
    radioactivity areas with the potential for individual worker internal exposures:
remote job coverage), and contamination controls. The inspectors evaluated the  
    *       RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
licensees use of electronic personal dosimeters in high noise areas as high radiation  
    *       RWP 141148; U1C26 - Steam Generator Platform Activities; and
area monitoring devices.  
    *       RWP 141145; U1C26 - Valve Maintenance / Repair.
The inspectors reviewed the application of dosimetry to effectively monitor exposure to  
    For these radiation work permits, the inspectors evaluated airborne radioactive controls
personnel in high-radiation work areas with significant dose rate gradients.  
    and monitoring, including potential for significant airborne levels (e.g., grinding, grit
The inspectors reviewed the following radiation work permits for work within airborne  
    blasting, system breaches, entry into tanks, cubicles, and reactor cavities). The
radioactivity areas with the potential for individual worker internal exposures:  
    inspectors assessed barrier (e.g., tent or glove box) integrity and temporary
*  
    high-efficiency particulate air ventilation system operation.
RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;
                                                33
*  
RWP 141148; U1C26 - Steam Generator Platform Activities; and  
*  
RWP 141145; U1C26 - Valve Maintenance / Repair.  
For these radiation work permits, the inspectors evaluated airborne radioactive controls  
and monitoring, including potential for significant airborne levels (e.g., grinding, grit  
blasting, system breaches, entry into tanks, cubicles, and reactor cavities). The  
inspectors assessed barrier (e.g., tent or glove box) integrity and temporary  
high-efficiency particulate air ventilation system operation.  


  The inspectors examined the licensees physical and programmatic controls for highly
  activated or contaminated materials (i.e., nonfuel) stored within spent fuel and other
34
  storage pools. The inspectors assessed whether appropriate controls (i.e.,
  administrative and physical controls) were in place to preclude inadvertent removal of
The inspectors examined the licensees physical and programmatic controls for highly  
  these materials from the pool.
activated or contaminated materials (i.e., nonfuel) stored within spent fuel and other  
  The inspectors examined the posting and physical controls for selected high radiation
storage pools. The inspectors assessed whether appropriate controls (i.e.,  
  areas and very-high radiation areas to verify conformance with the occupational
administrative and physical controls) were in place to preclude inadvertent removal of  
  performance indicator.
these materials from the pool.  
b. Findings
The inspectors examined the posting and physical controls for selected high radiation  
  Failure to Identify Deficient Locked High Radiation Area Controls Due to Procedure
areas and very-high radiation areas to verify conformance with the occupational  
  Inadequacy
performance indicator.  
  Introduction: An NRC identified Green NCV of TS 5.4.1, Procedures, was identified for
b.  
  inadequate procedures used to verify Locked High Radiation Controls in the Unit 2
Findings  
  Containment.
Failure to Identify Deficient Locked High Radiation Area Controls Due to Procedure  
  Description: On July 24, 2014, the inspector walked down the Unit 2 containment cavity
Inadequacy  
  access ladder. At the time of the walkdown, the access to the cavity was posted LHRA
Introduction: An NRC identified Green NCV of TS 5.4.1, Procedures, was identified for  
  and had a ladder cage that functioned as a ladder lock device, in addition to a four-foot
inadequate procedures used to verify Locked High Radiation Controls in the Unit 2  
  high locked gate for access to the permanently installed cavity ladder. Discussions with
Containment.  
  Radiation Protection staff had identified that the ladder lock device was not in place in
Description: On July 24, 2014, the inspector walked down the Unit 2 containment cavity  
  March 2014. Additionally, it was established that the locking cage was not placed back
access ladder. At the time of the walkdown, the access to the cavity was posted LHRA  
  on the ladder following the refueling outage in October 2013 when the area was
and had a ladder cage that functioned as a ladder lock device, in addition to a four-foot  
  conservatively posted as a LHRA as the dose rates in the containment cavity were not in
high locked gate for access to the permanently installed cavity ladder. Discussions with  
  excess of 1000 millirem per hour at 30 centimeters. The inspector reviewed Survey
Radiation Protection staff had identified that the ladder lock device was not in place in  
  Number CNP-1311-0001, dated November 1, 2013, which was a survey of the Final
March 2014. Additionally, it was established that the locking cage was not placed back  
  Containment Cavity Survey following the last refueling outage. This survey confirmed
on the ladder following the refueling outage in October 2013 when the area was  
  that the highest dose in the accessible areas of the cavity were nominally 2400 millirem
conservatively posted as a LHRA as the dose rates in the containment cavity were not in  
  per hour on contact, and 500 millirem per hour at 30 centimeters from the source with
excess of 1000 millirem per hour at 30 centimeters. The inspector reviewed Survey  
  the highest readings in the cavity lift system pit area following the cavity
Number CNP-1311-0001, dated November 1, 2013, which was a survey of the Final  
  decontamination. These dose rates would not constitute a LHRA (greater than
Containment Cavity Survey following the last refueling outage. This survey confirmed  
  1000 millirem per hour at 30 centimeters.) The survey showed that the gate to the cavity
that the highest dose in the accessible areas of the cavity were nominally 2400 millirem  
  ladder was posted as a LHRA.
per hour on contact, and 500 millirem per hour at 30 centimeters from the source with  
  Licensee Procedure PMP-6010-RPP-003, High, Locked High, and VHRA Access,
the highest readings in the cavity lift system pit area following the cavity  
  Section 3.3.5, directs weekly LHRA and VHRA verifications. Additional procedure
decontamination. These dose rates would not constitute a LHRA (greater than
  guidance is provided in THG-026, Locked High Radiation Area, and Very-High Radiation
1000 millirem per hour at 30 centimeters.) The survey showed that the gate to the cavity  
  Weekly Verification Process, Data Sheet 1, LHRA/VHRA Status Sheet, with additional
ladder was posted as a LHRA.  
  management expectations and a tracking tool for door/gate verifications while used as a
Licensee Procedure PMP-6010-RPP-003, High, Locked High, and VHRA Access,  
  field guide for verifying LHRA/VHRA controls (i.e., doors/gates). The inspector identified
Section 3.3.5, directs weekly LHRA and VHRA verifications. Additional procedure  
  a substantial procedural weakness in this guidance in that the Data Sheet apparently did
guidance is provided in THG-026, Locked High Radiation Area, and Very-High Radiation  
  not provide enough detail to direct Radiation Protection Technicians (RPTs) to verify that
Weekly Verification Process, Data Sheet 1, LHRA/VHRA Status Sheet, with additional  
  the locked cage/ladder lock to the reactor cavity was in place and locked; a condition
management expectations and a tracking tool for door/gate verifications while used as a  
  which is necessary to provide reasonable assurance that the area is secured against
field guide for verifying LHRA/VHRA controls (i.e., doors/gates). The inspector identified  
  unauthorized access and cannot be easily circumvented. A review of the data verified
a substantial procedural weakness in this guidance in that the Data Sheet apparently did  
  that RP staff did not identify the missing cage/ladder lock to the Unit 2 Reactor Cavity
not provide enough detail to direct Radiation Protection Technicians (RPTs) to verify that  
  ladder during weekly LHRA verification from November 2013 through March 2014. The
the locked cage/ladder lock to the reactor cavity was in place and locked; a condition  
  NRC inspectors also reviewed the LHRA and VHRA verification documentation in the
which is necessary to provide reasonable assurance that the area is secured against  
                                              34
unauthorized access and cannot be easily circumvented. A review of the data verified  
that RP staff did not identify the missing cage/ladder lock to the Unit 2 Reactor Cavity  
ladder during weekly LHRA verification from November 2013 through March 2014. The  
NRC inspectors also reviewed the LHRA and VHRA verification documentation in the  


RP station daily logs from November 2013 to March 2014 and the inspectors did not
identify any discrepancies noted in the logs associated with in LHRA controls during their
35
weekly walkdowns of LHRA and VHRA verification. A review of the Corrective Action
Program documents did not identify a record of the missing ladder lock device or
RP station daily logs from November 2013 to March 2014 and the inspectors did not  
identification of an unlocked LHRA. Therefore the licensee was not aware of the
identify any discrepancies noted in the logs associated with in LHRA controls during their  
deficient LHRA controls at the Unit 2 cavity ladder until it was discussed with the
weekly walkdowns of LHRA and VHRA verification. A review of the Corrective Action  
inspectors. The failure to identify deficient LHRA controls could have the potential failure
Program documents did not identify a record of the missing ladder lock device or  
to identify and report a Performance Indicator (PI) occurrence.
identification of an unlocked LHRA. Therefore the licensee was not aware of the  
Analysis: The inspectors determined that there was an inadequacy in the licensees
deficient LHRA controls at the Unit 2 cavity ladder until it was discussed with the  
procedure for identifying a deficient Locked High Radiation Area for the barrier in their
inspectors. The failure to identify deficient LHRA controls could have the potential failure  
weekly locked cage/ladder barrier to the cavity of Unit 2 containment. The inspectors
to identify and report a Performance Indicator (PI) occurrence.  
determined that the procedure did not provide clear directions to assure the Radiation
Analysis: The inspectors determined that there was an inadequacy in the licensees  
Protection Technician would verify the required controls for LHRA is a performance
procedure for identifying a deficient Locked High Radiation Area for the barrier in their  
deficiency. The inspectors determined that the cause of the performance deficiency was
weekly locked cage/ladder barrier to the cavity of Unit 2 containment. The inspectors  
reasonably within the licensees ability to foresee and correct and should have been
determined that the procedure did not provide clear directions to assure the Radiation  
prevented.
Protection Technician would verify the required controls for LHRA is a performance  
The finding was not subject to traditional enforcement since the incident did not have a
deficiency. The inspectors determined that the cause of the performance deficiency was  
significant safety consequence, did not impact the NRCs ability to perform its regulatory
reasonably within the licensees ability to foresee and correct and should have been  
function, and was not willful.
prevented.  
The inspectors determined that the performance deficiency was more than minor in
The finding was not subject to traditional enforcement since the incident did not have a  
accordance with IMC 0612, Appendix B, Issue Screening, because if left uncorrected,
significant safety consequence, did not impact the NRCs ability to perform its regulatory  
the performance deficiency could lead to a more significant safety concern. Specifically,
function, and was not willful.  
the failure to identify deficient LHRA controls could result in unintentional exposure to
The inspectors determined that the performance deficiency was more than minor in  
high levels of radiation.
accordance with IMC 0612, Appendix B, Issue Screening, because if left uncorrected,  
The finding was assessed using the Occupational Radiation Safety SDP and was
the performance deficiency could lead to a more significant safety concern. Specifically,  
determined to be of very-low safety significance because the problem was not an
the failure to identify deficient LHRA controls could result in unintentional exposure to  
ALARA planning issue, there were no overexposures nor substantial potential for
high levels of radiation.  
overexposures given the highest dose rates present in the room, the scope of work, and
The finding was assessed using the Occupational Radiation Safety SDP and was  
the licensees ability to assess dose was not compromised.
determined to be of very-low safety significance because the problem was not an  
The inspectors did not identify a corresponding cross-cutting aspect for this performance
ALARA planning issue, there were no overexposures nor substantial potential for  
deficiency.
overexposures given the highest dose rates present in the room, the scope of work, and  
Enforcement: Technical Specification 5.4.1, Procedures, requires that written
the licensees ability to assess dose was not compromised.  
procedures shall be established, implemented and maintained covering the activities
The inspectors did not identify a corresponding cross-cutting aspect for this performance  
referenced in Appendix A of Regulatory Guide 1.33, Revision 2. Control of Radioactivity
deficiency.  
procedures, including limiting personnel exposure, are specified in Appendix A.
Enforcement: Technical Specification 5.4.1, Procedures, requires that written  
Contrary to the above, Procedure PMP-6010-RPP-003, High, Locked High, and
procedures shall be established, implemented and maintained covering the activities  
Very-High Radiation Area Access, Section 3.3.5, LHRA and VHRA Door/Gate
referenced in Appendix A of Regulatory Guide 1.33, Revision 2. Control of Radioactivity  
verification in conjunction with Procedural Guidance THG-026, Locked High Radiation
procedures, including limiting personnel exposure, are specified in Appendix A.  
Area, and Very-High Radiation Weekly Verification Process did not provide sufficient
Contrary to the above, Procedure PMP-6010-RPP-003, High, Locked High, and  
details to direct RPTs to verify that the locked cage/ladder lock to the reactor cavity was
Very-High Radiation Area Access, Section 3.3.5, LHRA and VHRA Door/Gate  
in place and locked; a condition which is necessary to provide reasonable assurance
verification in conjunction with Procedural Guidance THG-026, Locked High Radiation  
that the area is secured against unauthorized access and cannot be easily
Area, and Very-High Radiation Weekly Verification Process did not provide sufficient  
circumvented. Consequently, weekly, from November 1, 2013, to March 2014 multiple
details to direct RPTs to verify that the locked cage/ladder lock to the reactor cavity was  
                                          35
in place and locked; a condition which is necessary to provide reasonable assurance  
that the area is secured against unauthorized access and cannot be easily  
circumvented. Consequently, weekly, from November 1, 2013, to March 2014 multiple  


    RPTs verified the Unit 2 Upper Containment Cavity gate was locked, but did not secure
    the area against unauthorized access.
36
    Corrective actions included review and revision of Procedure PMP-6010-RPP-003, High,
    Locked High, and Very-High Radiation Area Access, and the associated Procedural
RPTs verified the Unit 2 Upper Containment Cavity gate was locked, but did not secure  
    Guidance THG-026, Locked High Radiation Area and Very-High Radiation Weekly
the area against unauthorized access.  
    Verification. Because this violation is of very-low safety significance and it was entered
Corrective actions included review and revision of Procedure PMP-6010-RPP-003, High,  
    into the licensees CAP as AR 2014-9001, this violation is being treated as an NCV
Locked High, and Very-High Radiation Area Access, and the associated Procedural  
    consistent with Section 2.3.2 of the NRC Enforcement Policy.
Guidance THG-026, Locked High Radiation Area and Very-High Radiation Weekly  
    (NCV 05000315/2014005-06; 05000316/2014005-06; Failure to Identify Deficient
Verification. Because this violation is of very-low safety significance and it was entered  
    Locked High Radiation Area Controls Due to Procedure Inadequacy)
into the licensees CAP as AR 2014-9001, this violation is being treated as an NCV  
.5   Risk Significant High Radiation Area and Very-High Radiation Area Controls (02.06)
consistent with Section 2.3.2 of the NRC Enforcement Policy.  
  a. Inspection Scope
(NCV 05000315/2014005-06; 05000316/2014005-06; Failure to Identify Deficient  
    The inspectors discussed with the radiation protection manager the controls and
Locked High Radiation Area Controls Due to Procedure Inadequacy)  
    procedures for high-risk, high radiation areas and very-high radiation areas. The
.5  
    inspectors discussed methods employed by the licensee to provide stricter control of
Risk Significant High Radiation Area and Very-High Radiation Area Controls (02.06)  
    very-high radiation area access as specified in 10 CFR 20.1602, Control of Access to
a.  
    Very-High Radiation Areas, and Regulatory Guide 8.38, Control of Access to High and
Inspection Scope  
    Very-High Radiation Areas of Nuclear Plants. The inspectors assessed whether any
The inspectors discussed with the radiation protection manager the controls and  
    changes to licensee procedures substantially reduce the effectiveness and level of
procedures for high-risk, high radiation areas and very-high radiation areas. The  
    worker protection.
inspectors discussed methods employed by the licensee to provide stricter control of  
    The inspectors discussed the controls in place for special areas that have the potential
very-high radiation area access as specified in 10 CFR 20.1602, Control of Access to  
    to become very-high radiation areas during certain plant operations with first-line health
Very-High Radiation Areas, and Regulatory Guide 8.38, Control of Access to High and  
    physics supervisors (or equivalent positions having backshift health physics oversight
Very-High Radiation Areas of Nuclear Plants. The inspectors assessed whether any  
    authority). The inspectors assessed whether these plant operations require
changes to licensee procedures substantially reduce the effectiveness and level of  
    communication beforehand with the health physics group, so as to allow corresponding
worker protection.  
    timely actions to properly post, control, and monitor the radiation hazards including
The inspectors discussed the controls in place for special areas that have the potential  
    re-access authorization.
to become very-high radiation areas during certain plant operations with first-line health  
    The inspectors evaluated licensee controls for very-high radiation areas and areas with
physics supervisors (or equivalent positions having backshift health physics oversight  
    the potential to become a very-high radiation areas to ensure that an individual was not
authority). The inspectors assessed whether these plant operations require  
    able to gain unauthorized access to the very-high radiation areas.
communication beforehand with the health physics group, so as to allow corresponding  
  b. Findings
timely actions to properly post, control, and monitor the radiation hazards including  
    No findings were identified.
re-access authorization.  
.6   Radiation Worker Performance (02.07)
The inspectors evaluated licensee controls for very-high radiation areas and areas with  
  a. Inspection Scope
the potential to become a very-high radiation areas to ensure that an individual was not  
    The inspectors observed radiation worker performance with respect to stated radiation
able to gain unauthorized access to the very-high radiation areas.  
    protection work requirements. The inspectors assessed whether workers were aware of
b.  
    the radiological conditions in their workplace and the radiation work permit controls/limits
Findings  
    in place, and whether their performance reflected the level of radiological hazards
No findings were identified.  
    present.
.6  
                                              36
Radiation Worker Performance (02.07)  
a.  
Inspection Scope  
The inspectors observed radiation worker performance with respect to stated radiation  
protection work requirements. The inspectors assessed whether workers were aware of  
the radiological conditions in their workplace and the radiation work permit controls/limits  
in place, and whether their performance reflected the level of radiological hazards  
present.  


  b. Findings
      No findings were identified.
37
.7   Radiation Protection Technician Proficiency (02.08)
  a. Inspection Scope
b.  
      The inspectors observed the performance of the radiation protection technicians with
Findings  
      respect to all radiation protection work requirements. The inspectors evaluated whether
No findings were identified.  
      technicians were aware of the radiological conditions in their workplace and the radiation
.7  
      work permit controls/limits, and whether their performance was consistent with their
Radiation Protection Technician Proficiency (02.08)  
      training and qualifications with respect to the radiological hazards and work activities.
a.  
  b. Findings
Inspection Scope  
      No findings were identified.
The inspectors observed the performance of the radiation protection technicians with  
.8   Problem Identification and Resolution (02.09)
respect to all radiation protection work requirements. The inspectors evaluated whether  
  a. Inspection Scope
technicians were aware of the radiological conditions in their workplace and the radiation  
      The inspectors evaluated whether problems associated with radiation monitoring and
work permit controls/limits, and whether their performance was consistent with their  
      exposure control were being identified by the licensee at an appropriate threshold and
training and qualifications with respect to the radiological hazards and work activities.  
      were properly addressed for resolution in the licensees Corrective Action Program. The
b.  
      inspectors assessed the appropriateness of the corrective actions for a selected sample
Findings  
      of problems documented by the licensee that involve radiation monitoring and exposure
No findings were identified.  
      controls. The inspectors assessed the licensees process for applying operating
.8  
      experience to their plant.
Problem Identification and Resolution (02.09)  
  b. Findings
a.  
      No findings were identified.
Inspection Scope  
2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02)
The inspectors evaluated whether problems associated with radiation monitoring and  
      The inspection activities supplement those documented in NRC Inspection Report
exposure control were being identified by the licensee at an appropriate threshold and  
      05000315-05000316/2014002 and constitute a partial sample as defined in Inspection
were properly addressed for resolution in the licensees Corrective Action Program. The  
      Procedure 71124.02-05.
inspectors assessed the appropriateness of the corrective actions for a selected sample  
.1   Radiation Worker Performance (02.05)
of problems documented by the licensee that involve radiation monitoring and exposure  
  a. Inspection Scope
controls. The inspectors assessed the licensees process for applying operating  
      The inspectors observed radiation worker and radiation protection technician
experience to their plant.  
      performance during work activities being performed in radiation areas, airborne
b.  
      radioactivity areas, or high radiation areas. The inspectors evaluated whether workers
Findings  
      demonstrated the ALARA philosophy in practice (e.g., workers are familiar with the work
No findings were identified.  
      activity scope and tools to be used, workers used ALARA low-dose waiting areas) and
2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02)  
      whether there were any procedure compliance issues (e.g., workers are not complying
The inspection activities supplement those documented in NRC Inspection Report  
      with work activity controls). The inspectors observed radiation worker performance to
05000315-05000316/2014002 and constitute a partial sample as defined in Inspection  
      assess whether the training and skill level was sufficient with respect to the radiological
Procedure 71124.02-05.  
      hazards and the work involved.
.1  
                                                37
Radiation Worker Performance (02.05)  
a.  
Inspection Scope  
The inspectors observed radiation worker and radiation protection technician  
performance during work activities being performed in radiation areas, airborne  
radioactivity areas, or high radiation areas. The inspectors evaluated whether workers  
demonstrated the ALARA philosophy in practice (e.g., workers are familiar with the work  
activity scope and tools to be used, workers used ALARA low-dose waiting areas) and  
whether there were any procedure compliance issues (e.g., workers are not complying  
with work activity controls). The inspectors observed radiation worker performance to  
assess whether the training and skill level was sufficient with respect to the radiological  
hazards and the work involved.  


  b. Findings
      No findings were identified.
38
2RS7 Radiological Environmental Monitoring Program (71124.07)
      This inspection constituted one complete sample as defined in Inspection Procedure
b.  
      71124.07-05.
Findings  
.1   Inspection Planning (02.01)
No findings were identified.  
  a. Inspection Scope
2RS7 Radiological Environmental Monitoring Program (71124.07)  
      The inspectors reviewed the annual radiological environmental operating reports and the
This inspection constituted one complete sample as defined in Inspection Procedure  
      results of any licensee assessments since the last inspection to assess whether the
71124.07-05.  
      Radiological Environmental Monitoring Program was implemented in accordance with
.1  
      the Technical Specifications and Offsite Dose Calculation Manual. This review included
Inspection Planning (02.01)  
      reported changes to the Offsite Dose Calculation Manual with respect to environmental
a.  
      monitoring, commitments in terms of sampling locations, monitoring and measurement
Inspection Scope  
      frequencies, land use census, Inter-Laboratory Comparison Program, and analysis of
The inspectors reviewed the annual radiological environmental operating reports and the  
      data.
results of any licensee assessments since the last inspection to assess whether the  
      The inspectors reviewed the Offsite Dose Calculation Manual to identify locations of
Radiological Environmental Monitoring Program was implemented in accordance with  
      environmental monitoring stations.
the Technical Specifications and Offsite Dose Calculation Manual. This review included  
      The inspectors reviewed the Final Safety Analysis Report for information regarding the
reported changes to the Offsite Dose Calculation Manual with respect to environmental  
      environmental monitoring program and meteorological monitoring instrumentation.
monitoring, commitments in terms of sampling locations, monitoring and measurement  
      The inspectors reviewed quality assurance audit results of the program to assist in
frequencies, land use census, Inter-Laboratory Comparison Program, and analysis of  
      choosing inspection smart samples. The inspectors also reviewed audits and technical
data.  
      evaluations performed on the vendor laboratory if used.
The inspectors reviewed the Offsite Dose Calculation Manual to identify locations of  
      The inspectors reviewed the annual effluent release report and the 10 CFR Part 61,
environmental monitoring stations.  
      Licensing Requirements for Land Disposal of Radioactive Waste, report, to determine if
The inspectors reviewed the Final Safety Analysis Report for information regarding the  
      the licensee was sampling, as appropriate, for the predominant and dose-causing
environmental monitoring program and meteorological monitoring instrumentation.  
      radionuclides likely to be released in effluents.
The inspectors reviewed quality assurance audit results of the program to assist in  
  b. Findings
choosing inspection smart samples. The inspectors also reviewed audits and technical  
      No findings were identified.
evaluations performed on the vendor laboratory if used.  
.2   Site Inspection (02.02)
The inspectors reviewed the annual effluent release report and the 10 CFR Part 61,  
  a. Inspection Scope
Licensing Requirements for Land Disposal of Radioactive Waste, report, to determine if  
      The inspectors walked down select air sampling stations and dosimeter monitoring
the licensee was sampling, as appropriate, for the predominant and dose-causing  
      stations to determine whether they were located as described in the Offsite Dose
radionuclides likely to be released in effluents.  
      Calculation Manual and to determine the equipment material condition. Consistent with
b.  
      smart sampling, the air sampling stations were selected based on the locations with the
Findings  
      highest X/Q, D/Q wind sectors, and dosimeters were selected based on the most risk
No findings were identified.  
      significant locations (e.g., those that have the highest potential for public dose impact).
.2  
                                                38
Site Inspection (02.02)  
a.  
Inspection Scope  
The inspectors walked down select air sampling stations and dosimeter monitoring  
stations to determine whether they were located as described in the Offsite Dose  
Calculation Manual and to determine the equipment material condition. Consistent with  
smart sampling, the air sampling stations were selected based on the locations with the  
highest X/Q, D/Q wind sectors, and dosimeters were selected based on the most risk  
significant locations (e.g., those that have the highest potential for public dose impact).  


For the air samplers and dosimeters selected, the inspectors reviewed the calibration
and maintenance records to evaluate whether they demonstrated adequate operability of
39
these components. Additionally, the review included the calibration and maintenance
records of select composite water samplers.
For the air samplers and dosimeters selected, the inspectors reviewed the calibration  
The inspectors assessed whether the licensee had initiated sampling of other
and maintenance records to evaluate whether they demonstrated adequate operability of  
appropriate media upon loss of a required sampling station.
these components. Additionally, the review included the calibration and maintenance  
The inspectors observed the collection and preparation of environmental samples from
records of select composite water samplers.  
different environmental media (e.g., ground and surface water, milk, vegetation,
The inspectors assessed whether the licensee had initiated sampling of other  
sediment, and soil) as available to determine whether environmental sampling was
appropriate media upon loss of a required sampling station.  
representative of the release pathways as specified in the Offsite Dose Calculation
The inspectors observed the collection and preparation of environmental samples from  
Manual and if sampling techniques were in accordance with procedures.
different environmental media (e.g., ground and surface water, milk, vegetation,  
Based on direct observation and review of records, the inspectors assessed whether
sediment, and soil) as available to determine whether environmental sampling was  
the meteorological instruments were operable, calibrated, and maintained in
representative of the release pathways as specified in the Offsite Dose Calculation  
accordance with guidance contained in the Final Safety Analysis Report, NRC
Manual and if sampling techniques were in accordance with procedures.  
Regulatory Guide 1.23, Meteorological Monitoring Programs for Nuclear Power Plants,
Based on direct observation and review of records, the inspectors assessed whether  
and licensee procedures. The inspectors assessed whether the meteorological data
the meteorological instruments were operable, calibrated, and maintained in  
readout and recording instruments in the control room and, if applicable, at the tower
accordance with guidance contained in the Final Safety Analysis Report, NRC  
were operable.
Regulatory Guide 1.23, Meteorological Monitoring Programs for Nuclear Power Plants,  
The inspectors evaluated whether missed and/or anomalous environmental samples
and licensee procedures. The inspectors assessed whether the meteorological data  
were identified and reported in the annual environmental monitoring report. The
readout and recording instruments in the control room and, if applicable, at the tower  
inspectors selected events that involved a missed sample, inoperable sampler, lost
were operable.  
dosimeter, or anomalous measurement to determine if the licensee had identified the
The inspectors evaluated whether missed and/or anomalous environmental samples  
cause and had implemented corrective actions. The inspectors reviewed the licensees
were identified and reported in the annual environmental monitoring report. The  
assessment of any positive sample results (i.e., licensed radioactive material detected
inspectors selected events that involved a missed sample, inoperable sampler, lost  
above the lower limits of detection) and reviewed the associated radioactive effluent
dosimeter, or anomalous measurement to determine if the licensee had identified the  
release data that was the source of the released material.
cause and had implemented corrective actions. The inspectors reviewed the licensees  
The inspectors selected structures, systems, or components that involve or could
assessment of any positive sample results (i.e., licensed radioactive material detected  
reasonably involve licensed material for which there is a credible mechanism for
above the lower limits of detection) and reviewed the associated radioactive effluent  
licensed material to reach ground water, and assessed whether the licensee had
release data that was the source of the released material.  
implemented a sampling and monitoring program sufficient to detect leakage of these
The inspectors selected structures, systems, or components that involve or could  
structures, systems, or components to ground water.
reasonably involve licensed material for which there is a credible mechanism for  
The inspectors evaluated whether records, as required by 10 CFR 50.75(g), of leaks,
licensed material to reach ground water, and assessed whether the licensee had  
spills, and remediation since the previous inspection were retained in a retrievable
implemented a sampling and monitoring program sufficient to detect leakage of these  
manner.
structures, systems, or components to ground water.  
The inspectors reviewed any significant changes made by the licensee to the Offsite
The inspectors evaluated whether records, as required by 10 CFR 50.75(g), of leaks,  
Dose Calculation Manual as the result of changes to the land census, long-term
spills, and remediation since the previous inspection were retained in a retrievable  
meteorological conditions (3-year average), or modifications to the sampler stations
manner.  
since the last inspection. They reviewed technical justifications for any changed
The inspectors reviewed any significant changes made by the licensee to the Offsite  
sampling locations to evaluate whether the licensee performed the reviews required to
Dose Calculation Manual as the result of changes to the land census, long-term  
ensure that the changes did not affect its ability to monitor the impacts of radioactive
meteorological conditions (3-year average), or modifications to the sampler stations  
effluent releases on the environment.
since the last inspection. They reviewed technical justifications for any changed  
The inspectors assessed whether the appropriate detection sensitivities with respect to
sampling locations to evaluate whether the licensee performed the reviews required to  
Technical Specifications/Offsite Dose Calculation Manual where used for counting
ensure that the changes did not affect its ability to monitor the impacts of radioactive  
                                        39
effluent releases on the environment.  
The inspectors assessed whether the appropriate detection sensitivities with respect to  
Technical Specifications/Offsite Dose Calculation Manual where used for counting  


      samples (i.e., the samples meet the technical specifications/Offsite Dose Calculation
      Manual required lower limits of detection). The inspectors reviewed quality control
40
      charts for maintaining radiation measurement instrument status and actions taken for
      degrading detector performance. The licensee uses a vendor laboratory to analyze the
samples (i.e., the samples meet the technical specifications/Offsite Dose Calculation  
      radiological environmental monitoring program samples so the inspectors reviewed the
Manual required lower limits of detection). The inspectors reviewed quality control  
      results of the vendors quality control program, including the inter-laboratory comparison,
charts for maintaining radiation measurement instrument status and actions taken for  
      to assess the adequacy of the vendors program.
degrading detector performance. The licensee uses a vendor laboratory to analyze the  
      The inspectors reviewed the results of the licensees Inter-Laboratory Comparison
radiological environmental monitoring program samples so the inspectors reviewed the  
      Program to evaluate the adequacy of environmental sample analyses performed by the
results of the vendors quality control program, including the inter-laboratory comparison,  
      licensee. The inspectors assessed whether the inter-laboratory comparison test
to assess the adequacy of the vendors program.  
      included the media/nuclide mix appropriate for the facility. If applicable, the inspectors
The inspectors reviewed the results of the licensees Inter-Laboratory Comparison  
      reviewed the licensees determination of any bias to the data and the overall effect on
Program to evaluate the adequacy of environmental sample analyses performed by the  
      the radiological environmental monitoring program.
licensee. The inspectors assessed whether the inter-laboratory comparison test  
  b. Findings
included the media/nuclide mix appropriate for the facility. If applicable, the inspectors  
      No findings were identified.
reviewed the licensees determination of any bias to the data and the overall effect on  
.3   Identification and Resolution of Problems (02.03)
the radiological environmental monitoring program.  
  a. Inspection Scope
b.  
      The inspectors assessed whether problems associated with the radiological
Findings  
      environmental monitoring program were being identified by the licensee at an
No findings were identified.  
      appropriate threshold and were properly addressed for resolution in the licensees
.3  
      Corrective Action Program. Additionally, they assessed the appropriateness of the
Identification and Resolution of Problems (02.03)  
      corrective actions for a selected sample of problems documented by the licensee that
a.  
      involved the radiological environmental monitoring program.
Inspection Scope  
  b. Findings
The inspectors assessed whether problems associated with the radiological  
      No findings were identified.
environmental monitoring program were being identified by the licensee at an  
4.   OTHER ACTIVITIES
appropriate threshold and were properly addressed for resolution in the licensees  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
Corrective Action Program. Additionally, they assessed the appropriateness of the  
      Preparedness, and Occupational and Public Radiation Safety
corrective actions for a selected sample of problems documented by the licensee that  
4OA1 Performance Indicator Verification (71151)
involved the radiological environmental monitoring program.  
.1   Mitigating Systems Performance Index - Emergency AC Power System
b.  
  a. Inspection Scope
Findings  
      In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
No findings were identified.  
      Systems Performance Index (MSPI) - Emergency AC Power System performance
4.  
      indicator for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013
OTHER ACTIVITIES  
      through the second quarter 2014. To determine the accuracy of the PI data reported
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
      during those periods, PI definitions and guidance contained in the Nuclear Energy
Preparedness, and Occupational and Public Radiation Safety  
      Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
4OA1 Performance Indicator Verification (71151)  
      Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the
.1  
                                                40
Mitigating Systems Performance Index - Emergency AC Power System  
a.  
Inspection Scope  
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating  
Systems Performance Index (MSPI) - Emergency AC Power System performance  
indicator for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013  
through the second quarter 2014. To determine the accuracy of the PI data reported  
during those periods, PI definitions and guidance contained in the Nuclear Energy  
Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator  
Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the  


    licensees operator narrative logs, MSPI derivation reports, issue reports, event reports
    and NRC Integrated Inspection Reports for the period of July 2013 through June 2014 to
41
    validate the accuracy of the submittals. The inspectors reviewed the MSPI component
    risk coefficient to determine if it had changed by more than 25 percent in value since the
licensees operator narrative logs, MSPI derivation reports, issue reports, event reports  
    previous inspection, and if so, that the change was in accordance with applicable
and NRC Integrated Inspection Reports for the period of July 2013 through June 2014 to  
    NEI guidance. The inspectors also reviewed the licensees issue report database to
validate the accuracy of the submittals. The inspectors reviewed the MSPI component  
    determine if any problems had been identified with the PI data collected or transmitted
risk coefficient to determine if it had changed by more than 25 percent in value since the  
    for this indicator and none were identified. Documents reviewed are listed in the
previous inspection, and if so, that the change was in accordance with applicable  
    Attachment to this report. Portions of this inspection activity were credited in NRC
NEI guidance. The inspectors also reviewed the licensees issue report database to  
    Inspection Report 05000315-05000316/2014004.
determine if any problems had been identified with the PI data collected or transmitted  
    This inspection constituted one MSPI emergency AC power system sample as defined in
for this indicator and none were identified. Documents reviewed are listed in the  
    IP 71151-05.
Attachment to this report. Portions of this inspection activity were credited in NRC  
  b. Findings
Inspection Report 05000315-05000316/2014004.  
    No findings were identified.
This inspection constituted one MSPI emergency AC power system sample as defined in  
.2   Mitigating Systems Performance Index - High Pressure Injection Systems
IP 71151-05.  
  a. Inspection Scope
b.  
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
Findings  
    Systems Performance Index - High Pressure Injection Systems performance indicator
No findings were identified.  
    for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter of 2013 thru
.2  
    the third quarter of 2014. To determine the accuracy of the PI data reported during
Mitigating Systems Performance Index - High Pressure Injection Systems  
    those periods, PI definitions and guidance contained in the NEI Document 99-02,
a.  
    Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31,
Inspection Scope  
    2013, were used. The inspectors reviewed the licensees operator narrative logs, issue
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating  
    reports, MSPI derivation reports, event reports and NRC Integrated Inspection Reports
Systems Performance Index - High Pressure Injection Systems performance indicator  
    for the period of the third quarter of 2013 thru the 2nd quarter of 2014 to validate the
for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter of 2013 thru  
    accuracy of the submittals. The inspectors reviewed the MSPI component risk
the third quarter of 2014. To determine the accuracy of the PI data reported during  
    coefficient to determine if it had changed by more than 25 percent in value since the
those periods, PI definitions and guidance contained in the NEI Document 99-02,  
    previous inspection, and if so, that the change was in accordance with applicable
Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31,  
    NEI guidance. The inspectors also reviewed the licensees issue report database to
2013, were used. The inspectors reviewed the licensees operator narrative logs, issue  
    determine if any problems had been identified with the PI data collected or transmitted
reports, MSPI derivation reports, event reports and NRC Integrated Inspection Reports  
    for this indicator and none were identified. Documents reviewed are listed in the
for the period of the third quarter of 2013 thru the 2nd quarter of 2014 to validate the  
    Attachment to this report. Portions of this inspection activity were credited in NRC
accuracy of the submittals. The inspectors reviewed the MSPI component risk  
    Inspection Report 05000315-05000316/2014004.
coefficient to determine if it had changed by more than 25 percent in value since the  
    This inspection constituted one MSPI high pressure injection system sample as defined
previous inspection, and if so, that the change was in accordance with applicable  
    in IP 71151-05.
NEI guidance. The inspectors also reviewed the licensees issue report database to  
  b. Findings
determine if any problems had been identified with the PI data collected or transmitted  
    No findings were identified.
for this indicator and none were identified. Documents reviewed are listed in the  
                                                41
Attachment to this report. Portions of this inspection activity were credited in NRC  
Inspection Report 05000315-05000316/2014004.  
This inspection constituted one MSPI high pressure injection system sample as defined  
in IP 71151-05.  
b.  
Findings  
No findings were identified.  


.3   Mitigating Systems Performance Index - Heat Removal System
  a. Inspection Scope
42
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
    Systems Performance Index - Heat Removal System performance indicator for
.3  
    Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the
Mitigating Systems Performance Index - Heat Removal System  
    second quarter 2014. To determine the accuracy of the PI data reported during those
a.  
    periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
Inspection Scope  
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating  
    used. The inspectors reviewed the licensees operator narrative logs, issue reports,
Systems Performance Index - Heat Removal System performance indicator for
    event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the
Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the  
    period of July 2013 through June 2014 to validate the accuracy of the submittals. The
second quarter 2014. To determine the accuracy of the PI data reported during those  
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory  
    by more than 25 percent in value since the previous inspection, and if so, that the
Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were  
    change was in accordance with applicable NEI guidance. The inspectors also reviewed
used. The inspectors reviewed the licensees operator narrative logs, issue reports,  
    the licensees issue report database to determine if any problems had been identified
event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the  
    with the PI data collected or transmitted for this indicator and none were identified.
period of July 2013 through June 2014 to validate the accuracy of the submittals. The  
    Documents reviewed are listed in the Attachment to this report. Portions of this
inspectors reviewed the MSPI component risk coefficient to determine if it had changed  
    inspection activity were credited in NRC Inspection Report
by more than 25 percent in value since the previous inspection, and if so, that the  
    05000315-05000316/2014004.
change was in accordance with applicable NEI guidance. The inspectors also reviewed  
    This inspection constituted one MSPI heat removal system sample as defined in
the licensees issue report database to determine if any problems had been identified  
    IP 71151-05.
with the PI data collected or transmitted for this indicator and none were identified.
  b. Findings
Documents reviewed are listed in the Attachment to this report. Portions of this  
    No findings were identified.
inspection activity were credited in NRC Inspection Report  
.4   Mitigating Systems Performance Index - Residual Heat Removal System
05000315-05000316/2014004.  
  a. Inspection Scope
This inspection constituted one MSPI heat removal system sample as defined in  
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
IP 71151-05.  
    Systems Performance Index - Residual Heat Removal System performance indicator for
b.  
    Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the
Findings  
    second quarter 2014. To determine the accuracy of the PI data reported during those
No findings were identified.  
    periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
.4  
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
Mitigating Systems Performance Index - Residual Heat Removal System  
    used. The inspectors reviewed the licensees operator narrative logs, issue reports,
a.  
    MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the
Inspection Scope  
    period of July 2013 through June 2014 to validate the accuracy of the submittals. The
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating  
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
Systems Performance Index - Residual Heat Removal System performance indicator for  
    by more than 25 percent in value since the previous inspection, and if so, that the
Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the  
    change was in accordance with applicable NEI guidance. The inspectors also reviewed
second quarter 2014. To determine the accuracy of the PI data reported during those  
    the licensees issue report database to determine if any problems had been identified
periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory  
    with the PI data collected or transmitted for this indicator and none were identified.
Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were  
    Documents reviewed are listed in the Attachment to this report. Portions of this
used. The inspectors reviewed the licensees operator narrative logs, issue reports,  
    inspection activity were credited in NRC Inspection Report
MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the  
    05000315-05000316/2014004.
period of July 2013 through June 2014 to validate the accuracy of the submittals. The  
                                              42
inspectors reviewed the MSPI component risk coefficient to determine if it had changed  
by more than 25 percent in value since the previous inspection, and if so, that the  
change was in accordance with applicable NEI guidance. The inspectors also reviewed  
the licensees issue report database to determine if any problems had been identified  
with the PI data collected or transmitted for this indicator and none were identified.
Documents reviewed are listed in the Attachment to this report. Portions of this  
inspection activity were credited in NRC Inspection Report  
05000315-05000316/2014004.  


    This inspection constituted one MSPI residual heat removal system sample as defined in
    IP 71151-05.
43
  b. Findings
    No findings were identified.
This inspection constituted one MSPI residual heat removal system sample as defined in  
.5   Mitigating Systems Performance Index - Cooling Water Systems
IP 71151-05.  
  a. Inspection Scope
b.  
    In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating
Findings  
    Systems Performance Index - Cooling Water Systems performance indicator for
No findings were identified.  
    Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the
.5  
    second quarter 2014. To determine the accuracy of the PI data reported during those
Mitigating Systems Performance Index - Cooling Water Systems  
    periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory
a.  
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
Inspection Scope  
    used. The inspectors reviewed the licensees operator narrative logs, issue reports,
In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating  
    MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the
Systems Performance Index - Cooling Water Systems performance indicator for
    period of July 2013 through June 2014 to validate the accuracy of the submittals. The
Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the
    inspectors reviewed the MSPI component risk coefficient to determine if it had changed
second quarter 2014. To determine the accuracy of the PI data reported during those  
    by more than 25 percent in value since the previous inspection, and if so, that the
periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory  
    change was in accordance with applicable NEI guidance. The inspectors also reviewed
Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were  
    the licensees issue report database to determine if any problems had been identified
used. The inspectors reviewed the licensees operator narrative logs, issue reports,  
    with the PI data collected or transmitted for this indicator and none were identified.
MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the  
    Documents reviewed are listed in the Attachment to this report. Portions of this
period of July 2013 through June 2014 to validate the accuracy of the submittals. The  
    inspection activity were credited in NRC Inspection Report
inspectors reviewed the MSPI component risk coefficient to determine if it had changed  
    05000315-05000316/2014004.
by more than 25 percent in value since the previous inspection, and if so, that the  
    This inspection constituted one MSPI cooling water system sample as defined in
change was in accordance with applicable NEI guidance. The inspectors also reviewed  
    IP 71151-05.
the licensees issue report database to determine if any problems had been identified  
  b. Findings
with the PI data collected or transmitted for this indicator and none were identified.
    No findings were identified.
Documents reviewed are listed in the Attachment to this report. Portions of this  
.6   Reactor Coolant System Leakage
inspection activity were credited in NRC Inspection Report  
  a. Inspection Scope
05000315-05000316/2014004.  
    The inspectors sampled licensee submittals for the RCS Leakage performance indicator
This inspection constituted one MSPI cooling water system sample as defined in  
    for both Unit 1 and 2 for the period from the fourth quarter 2013 through the third quarter
IP 71151-05.  
    2014. To determine the accuracy of the PI data reported during those periods, PI
b.  
    definitions and guidance contained in the NEI Document 99-02, Regulatory
Findings  
    Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were
No findings were identified.  
    used. The inspectors reviewed the licensees operator logs, RCS leakage tracking data,
.6  
    issue reports, event reports and NRC Integrated Inspection Reports for the period of the
Reactor Coolant System Leakage  
    fourth quarter 2013 through the third quarter 2014 to validate the accuracy of the
a.  
    submittals. The inspectors also reviewed the licensees issue report database to
Inspection Scope  
    determine if any problems had been identified with the PI data collected or transmitted
The inspectors sampled licensee submittals for the RCS Leakage performance indicator  
    for this indicator and none were identified. Documents reviewed are listed in the
for both Unit 1 and 2 for the period from the fourth quarter 2013 through the third quarter  
    Attachment to this report.
2014. To determine the accuracy of the PI data reported during those periods, PI  
                                              43
definitions and guidance contained in the NEI Document 99-02, Regulatory  
Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were  
used. The inspectors reviewed the licensees operator logs, RCS leakage tracking data,  
issue reports, event reports and NRC Integrated Inspection Reports for the period of the  
fourth quarter 2013 through the third quarter 2014 to validate the accuracy of the  
submittals. The inspectors also reviewed the licensees issue report database to  
determine if any problems had been identified with the PI data collected or transmitted  
for this indicator and none were identified. Documents reviewed are listed in the  
Attachment to this report.  


    This inspection constituted two RCS leakage samples as defined in IP 71151-05.
  b. Findings
44
    No findings were identified.
.7   Reactor Coolant System Specific Activity
This inspection constituted two RCS leakage samples as defined in IP 71151-05.  
  a. Inspection Scope
b.  
    The inspectors sampled licensee submittals for the RCS specific activity Performance
Findings  
    Indicator for D.C. Cook Nuclear Power Plant Units 1 and 2 for the period from the third
No findings were identified.  
    quarter 2013 through the third quarter 2014. The inspectors used Performance Indicator
.7  
    definitions and guidance contained in the Nuclear Energy Institute Document 99-02,
Reactor Coolant System Specific Activity  
    Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August
a.  
    2013, to determine the accuracy of the Performance Indicator data reported during those
Inspection Scope  
    periods. The inspectors reviewed the licensees RCS chemistry samples, Technical
The inspectors sampled licensee submittals for the RCS specific activity Performance  
    Specification requirements, issue reports, event reports, and NRC Integrated Inspection
Indicator for D.C. Cook Nuclear Power Plant Units 1 and 2 for the period from the third  
    Reports to validate the accuracy of the submittals. The inspectors also reviewed the
quarter 2013 through the third quarter 2014. The inspectors used Performance Indicator  
    licensees issue report database to determine if any problems had been identified with
definitions and guidance contained in the Nuclear Energy Institute Document 99-02,  
    the Performance Indicator data collected or transmitted for this indicator and none were
Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August  
    identified. In addition to record reviews, the inspectors observed a chemistry technician
2013, to determine the accuracy of the Performance Indicator data reported during those  
    obtain and analyze a RCS sample. Documents reviewed are listed in the Attachment to
periods. The inspectors reviewed the licensees RCS chemistry samples, Technical  
    this report.
Specification requirements, issue reports, event reports, and NRC Integrated Inspection  
    This inspection constituted two RCS specific activity samples as defined in IP 71151-05.
Reports to validate the accuracy of the submittals. The inspectors also reviewed the  
  b. Findings
licensees issue report database to determine if any problems had been identified with  
    No findings were identified.
the Performance Indicator data collected or transmitted for this indicator and none were  
.8   Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
identified. In addition to record reviews, the inspectors observed a chemistry technician  
    Radiological Effluent Occurrences
obtain and analyze a RCS sample. Documents reviewed are listed in the Attachment to  
  a. Inspection Scope
this report.  
    The inspectors sampled licensee submittals for the radiological effluent Technical
This inspection constituted two RCS specific activity samples as defined in IP 71151-05.  
    Specification/Offsite Dose Calculation Manual radiological effluent occurrences
b.  
    Performance Indicator for the period from the third quarter 2013 through the third quarter
Findings  
    2014. The inspectors used Performance Indicator definitions and guidance contained in
No findings were identified.  
    the Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance
.8  
    Indicator Guideline, Revision 7, dated August 2013, to determine the accuracy of the
Radiological Effluent Technical Specification/Offsite Dose Calculation Manual  
    Performance Indicator data reported during those periods. The inspectors reviewed the
Radiological Effluent Occurrences  
    licensees issue report database and selected individual reports generated since this
a.  
    indicator was last reviewed to identify any potential occurrences such as unmonitored,
Inspection Scope  
    uncontrolled, or improperly calculated effluent releases that may have impacted offsite
The inspectors sampled licensee submittals for the radiological effluent Technical  
    dose. The inspectors reviewed gaseous effluent summary data and the results of
Specification/Offsite Dose Calculation Manual radiological effluent occurrences  
    associated offsite dose calculations for selected dates to determine if indicator results
Performance Indicator for the period from the third quarter 2013 through the third quarter  
    were accurately reported. The inspectors also reviewed the licensees methods for
2014. The inspectors used Performance Indicator definitions and guidance contained in  
    quantifying gaseous and liquid effluents and determining effluent dose. Documents
the Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance  
    reviewed are listed in the Attachment to this report.
Indicator Guideline, Revision 7, dated August 2013, to determine the accuracy of the  
                                              44
Performance Indicator data reported during those periods. The inspectors reviewed the  
licensees issue report database and selected individual reports generated since this  
indicator was last reviewed to identify any potential occurrences such as unmonitored,  
uncontrolled, or improperly calculated effluent releases that may have impacted offsite  
dose. The inspectors reviewed gaseous effluent summary data and the results of  
associated offsite dose calculations for selected dates to determine if indicator results  
were accurately reported. The inspectors also reviewed the licensees methods for  
quantifying gaseous and liquid effluents and determining effluent dose. Documents  
reviewed are listed in the Attachment to this report.  


      This inspection constituted one Radiological Effluent Technical Specification/Offsite
      Dose Calculation Manual radiological effluent occurrences sample as defined in
45
      IP 71151 05.
  b. Findings
This inspection constituted one Radiological Effluent Technical Specification/Offsite  
      No findings were identified.
Dose Calculation Manual radiological effluent occurrences sample as defined in  
.9   Occupational Exposure Control Effectiveness
IP 71151 05.  
  a. Inspection Scope
b.  
      The inspectors sampled licensee submittals for the Occupational Exposure Control
Findings  
      Effectiveness Performance Indicator for the period from the third quarter 2013 through
No findings were identified.  
      the third quarter 2014. The inspectors used Performance Indicator definitions and
.9  
      guidance contained in the Nuclear Energy Institute Document 99-02, Regulatory
Occupational Exposure Control Effectiveness  
      Assessment Performance Indicator Guideline, Revision 7, dated August 2013, to
a.  
      determine the accuracy of the Performance Indicator data reported during those periods.
Inspection Scope  
      The inspectors reviewed the licensees assessment of the Performance Indicator for
The inspectors sampled licensee submittals for the Occupational Exposure Control  
      occupational radiation safety to determine if the indicator related data was adequately
Effectiveness Performance Indicator for the period from the third quarter 2013 through  
      assessed and reported. To assess the adequacy of the licensees Performance
the third quarter 2014. The inspectors used Performance Indicator definitions and  
      Indicator data collection and analyses, the inspectors discussed with radiation protection
guidance contained in the Nuclear Energy Institute Document 99-02, Regulatory  
      staff the scope and breadth of its data review and the results of those reviews. The
Assessment Performance Indicator Guideline, Revision 7, dated August 2013, to  
      inspectors independently reviewed electronic personal dosimetry dose rate and
determine the accuracy of the Performance Indicator data reported during those periods.
      accumulated dose alarms and dose reports and the dose assignments for any intakes
The inspectors reviewed the licensees assessment of the Performance Indicator for  
      that occurred during the time period reviewed to determine if there were potentially
occupational radiation safety to determine if the indicator related data was adequately  
      unrecognized occurrences. The inspectors also conducted walkdowns of numerous
assessed and reported. To assess the adequacy of the licensees Performance  
      locked high and very-high radiation area entrances to determine the adequacy of the
Indicator data collection and analyses, the inspectors discussed with radiation protection  
      controls in place for these areas. Documents reviewed are listed in the Attachment to
staff the scope and breadth of its data review and the results of those reviews. The  
      this report.
inspectors independently reviewed electronic personal dosimetry dose rate and  
      This inspection constituted one occupational exposure control effectiveness sample as
accumulated dose alarms and dose reports and the dose assignments for any intakes  
      defined in IP 71151-05.
that occurred during the time period reviewed to determine if there were potentially  
  b. Findings
unrecognized occurrences. The inspectors also conducted walkdowns of numerous  
      No findings were identified.
locked high and very-high radiation area entrances to determine the adequacy of the  
4OA2 Identification and Resolution of Problems (71152)
controls in place for these areas. Documents reviewed are listed in the Attachment to  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
this report.  
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
This inspection constituted one occupational exposure control effectiveness sample as  
      Physical Protection
defined in IP 71151-05.  
.1   Routine Review of Items Entered into the Corrective Action Program
b.  
  a. Inspection Scope
Findings  
      As part of the various baseline inspection procedures discussed in previous sections of
No findings were identified.  
      this report, the inspectors routinely reviewed issues during baseline inspection activities
4OA2 Identification and Resolution of Problems (71152)  
      and plant status reviews to verify they were being entered into the licensees CAP at an
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
      appropriate threshold, that adequate attention was being given to timely corrective
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and  
                                                45
Physical Protection  
.1  
Routine Review of Items Entered into the Corrective Action Program  
a.  
Inspection Scope  
As part of the various baseline inspection procedures discussed in previous sections of  
this report, the inspectors routinely reviewed issues during baseline inspection activities  
and plant status reviews to verify they were being entered into the licensees CAP at an  
appropriate threshold, that adequate attention was being given to timely corrective  


    actions, and that adverse trends were identified and addressed. Attributes reviewed
    included: identification of the problem was complete and accurate; timeliness was
46
    commensurate with the safety significance; evaluation and disposition of performance
    issues, generic implications, common causes, contributing factors, root causes,
actions, and that adverse trends were identified and addressed. Attributes reviewed  
    extent-of-condition reviews, and previous occurrences reviews were proper and
included: identification of the problem was complete and accurate; timeliness was  
    adequate; and that the classification, prioritization, focus, and timeliness of corrective
commensurate with the safety significance; evaluation and disposition of performance  
    actions were commensurate with safety and sufficient to prevent recurrence of the issue.
issues, generic implications, common causes, contributing factors, root causes,  
    Minor issues entered into the licensees CAP as a result of the inspectors observations
extent-of-condition reviews, and previous occurrences reviews were proper and  
    are included in the Attachment to this report.
adequate; and that the classification, prioritization, focus, and timeliness of corrective  
    These routine reviews for the identification and resolution of problems did not constitute
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
    any additional inspection samples. Instead, by procedure they were considered an
Minor issues entered into the licensees CAP as a result of the inspectors observations  
    integral part of the inspections performed during the quarter and documented in
are included in the Attachment to this report.  
    Section 1 of this report.
These routine reviews for the identification and resolution of problems did not constitute  
  b. Findings
any additional inspection samples. Instead, by procedure they were considered an  
    No findings were identified.
integral part of the inspections performed during the quarter and documented in  
.2   Daily Corrective Action Program Reviews
Section 1 of this report.  
  a. Inspection Scope
b.  
    In order to assist with the identification of repetitive equipment failures and specific
Findings  
    human performance issues for followup, the inspectors performed a daily screening of
No findings were identified.  
    items entered into the licensees CAP. This review was accomplished through
.2  
    inspection of the stations daily condition report packages.
Daily Corrective Action Program Reviews  
    These daily reviews were performed by procedure as part of the inspectors daily plant
a.  
    status monitoring activities and, as such, did not constitute any separate inspection
Inspection Scope  
    samples.
In order to assist with the identification of repetitive equipment failures and specific  
  b. Findings
human performance issues for followup, the inspectors performed a daily screening of  
    No findings were identified.
items entered into the licensees CAP. This review was accomplished through  
.3   Semiannual Trend Review
inspection of the stations daily condition report packages.  
  a. Inspection Scope
These daily reviews were performed by procedure as part of the inspectors daily plant  
    The inspectors performed a review of the licensees CAP and associated documents to
status monitoring activities and, as such, did not constitute any separate inspection  
    identify trends that could indicate the existence of a more significant safety issue. The
samples.  
    inspectors review was focused on repetitive equipment issues, but also considered the
b.  
    results of daily inspector CAP item screening discussed in Section 4OA2.2 above,
Findings  
    licensee trending efforts, and licensee human performance results. The inspectors
No findings were identified.  
    review nominally considered the 6-month period of July 2014 through December 2014,
.3  
    although some examples expanded beyond those dates where the scope of the trend
Semiannual Trend Review  
    warranted.
a.  
    The review also included issues documented outside the normal CAP in major
Inspection Scope  
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
The inspectors performed a review of the licensees CAP and associated documents to  
    problem/challenges lists, system health reports, quality assurance audit/surveillance
identify trends that could indicate the existence of a more significant safety issue. The  
                                                46
inspectors review was focused on repetitive equipment issues, but also considered the  
results of daily inspector CAP item screening discussed in Section 4OA2.2 above,  
licensee trending efforts, and licensee human performance results. The inspectors  
review nominally considered the 6-month period of July 2014 through December 2014,  
although some examples expanded beyond those dates where the scope of the trend  
warranted.  
The review also included issues documented outside the normal CAP in major  
equipment problem lists, repetitive and/or rework maintenance lists, departmental  
problem/challenges lists, system health reports, quality assurance audit/surveillance  


    reports, self-assessment reports, and Maintenance Rule assessments. The inspectors
    compared and contrasted their results with the results contained in the licensees CAP
47
    trending reports. Corrective actions associated with a sample of the issues identified in
    the licensees trending reports were reviewed for adequacy.
reports, self-assessment reports, and Maintenance Rule assessments. The inspectors  
    The inspectors observed some weaknesses in different aspects of the operability
compared and contrasted their results with the results contained in the licensees CAP  
    determination process. There were some instances where ARs were written but were
trending reports. Corrective actions associated with a sample of the issues identified in  
    not flagged for an operability review. Some had been already identified by the licensee
the licensees trending reports were reviewed for adequacy.  
    upon questioning by the inspectors, others had not. In these cases, the inspectors did
The inspectors observed some weaknesses in different aspects of the operability  
    not find any instances where equipment should have been called inoperable but was
determination process. There were some instances where ARs were written but were  
    not. The inspectors also found a functionality assessment associated with fire pumps
not flagged for an operability review. Some had been already identified by the licensee  
    where necessary compensatory measures were not formalized until the inspectors had
upon questioning by the inspectors, others had not. In these cases, the inspectors did  
    questioned the assessment. During the period of review, there were two NRC identified
not find any instances where equipment should have been called inoperable but was  
    findings with identified weaknesses in the operability determination process. One was
not. The inspectors also found a functionality assessment associated with fire pumps  
    documented in NRC Inspection Report 2014004 and dealt with a failure to provide
where necessary compensatory measures were not formalized until the inspectors had  
    adequate technical justification for operability of a TDAFW pump with respect to
questioned the assessment. During the period of review, there were two NRC identified  
    governor oil levels. Another issue is documented in Section 1R15 of this report and
findings with identified weaknesses in the operability determination process. One was  
    dealt with, in part, appropriate oil levels for TDAFW bearings. The inspectors discussed
documented in NRC Inspection Report 2014004 and dealt with a failure to provide  
    the observations with licensee staff, who agreed with the assessment.
adequate technical justification for operability of a TDAFW pump with respect to  
    The inspectors also observed weaknesses in work planning and execution. Multiple
governor oil levels. Another issue is documented in Section 1R15 of this report and  
    instances were identified of scheduled work activities that had to be de-conflicted the
dealt with, in part, appropriate oil levels for TDAFW bearings. The inspectors discussed  
    day/week of execution. In some cases, procedures had to be revised to support work, or
the observations with licensee staff, who agreed with the assessment.  
    post-maintenance test activities changed to appropriately cover the scope of work near
The inspectors also observed weaknesses in work planning and execution. Multiple  
    time of execution. In some cases, where changes were made or expanded scope
instances were identified of scheduled work activities that had to be de-conflicted the  
    encountered, the plant risk summary sheet (a vehicle by which the plant risk is conveyed
day/week of execution. In some cases, procedures had to be revised to support work, or  
    to the site) was not updated appropriately. A finding in Section 1R15 of this report
post-maintenance test activities changed to appropriately cover the scope of work near  
    documents a case where inadequate planning and execution unexpectedly rendered a
time of execution. In some cases, where changes were made or expanded scope  
    diesel fuel oil storage tank inoperable. Inspectors have discussed the issue with
encountered, the plant risk summary sheet (a vehicle by which the plant risk is conveyed  
    licensee staff, who agreed with the assessment.
to the site) was not updated appropriately. A finding in Section 1R15 of this report  
    This review constituted one semiannual trend inspection sample as defined in
documents a case where inadequate planning and execution unexpectedly rendered a  
    IP 71152-05.
diesel fuel oil storage tank inoperable. Inspectors have discussed the issue with  
  b. Findings
licensee staff, who agreed with the assessment.  
    No findings were identified.
This review constituted one semiannual trend inspection sample as defined in
.4   Selected Issue Followup Inspection: Review of Operator Workarounds
IP 71152-05.  
  a. Inspection Scope
b.  
    The inspectors evaluated the licensees implementation of their process used to identify,
Findings  
    document, track, and resolve operational challenges. Inspection activities included, but
No findings were identified.  
    were not limited to, a review of the cumulative effects of the operator workarounds
.4  
    (OWAs) on system availability and the potential for improper operation of the system, for
Selected Issue Followup Inspection: Review of Operator Workarounds  
    potential impacts on multiple systems, and on the ability of operators to respond to plant
a.  
    transients or accidents.
Inspection Scope  
    The inspectors performed a review of the cumulative effects of OWAs. The documents
The inspectors evaluated the licensees implementation of their process used to identify,  
    listed in the Attachment to this report were reviewed to accomplish the objectives of the
document, track, and resolve operational challenges. Inspection activities included, but  
    inspection procedure. The inspectors reviewed both current and historical operational
were not limited to, a review of the cumulative effects of the operator workarounds  
                                                47
(OWAs) on system availability and the potential for improper operation of the system, for  
potential impacts on multiple systems, and on the ability of operators to respond to plant  
transients or accidents.  
The inspectors performed a review of the cumulative effects of OWAs. The documents  
listed in the Attachment to this report were reviewed to accomplish the objectives of the  
inspection procedure. The inspectors reviewed both current and historical operational  


    challenge records to determine whether the licensee was identifying operator challenges
    at an appropriate threshold, had entered them into their CAP and proposed or
48
    implemented appropriate and timely corrective actions which addressed each issue.
    Reviews were conducted to determine if any operator challenge could increase the
challenge records to determine whether the licensee was identifying operator challenges  
    possibility of an Initiating Event, if the challenge was contrary to training, required a
at an appropriate threshold, had entered them into their CAP and proposed or  
    change from long-standing operational practices, or created the potential for
implemented appropriate and timely corrective actions which addressed each issue.
    inappropriate compensatory actions. Additionally, all temporary modifications were
Reviews were conducted to determine if any operator challenge could increase the  
    reviewed to identify any potential effect on the functionality of Mitigating Systems,
possibility of an Initiating Event, if the challenge was contrary to training, required a  
    impaired access to equipment, or required equipment uses for which the equipment was
change from long-standing operational practices, or created the potential for  
    not designed. Daily plant and equipment status logs, degraded instrument logs, and
inappropriate compensatory actions. Additionally, all temporary modifications were  
    operator aids or tools being used to compensate for material deficiencies were also
reviewed to identify any potential effect on the functionality of Mitigating Systems,  
    assessed to identify any potential sources of unidentified operator workarounds.
impaired access to equipment, or required equipment uses for which the equipment was  
    This review constituted one in depth review of a selected issue sample (operator work
not designed. Daily plant and equipment status logs, degraded instrument logs, and  
    arounds) as defined in IP 71152-05.
operator aids or tools being used to compensate for material deficiencies were also  
  b. Findings
assessed to identify any potential sources of unidentified operator workarounds.  
    No findings were identified.
This review constituted one in depth review of a selected issue sample (operator work  
.5   Selected Issue Follow-up Inspection: Follow-up to Previous NRC Findings
arounds) as defined in IP 71152-05.  
  a. Inspection Scope
b.  
    The inspectors selected a sample of previously issued NRC findings to assess the
Findings  
    adequacy of licensee corrective actions. Two instances were identified where the
No findings were identified.  
    technical issues had been adequately addressed; however, it appeared there were no
.5  
    corrective actions for underlying performance issues. In one case, a finding was issued
Selected Issue Follow-up Inspection: Follow-up to Previous NRC Findings  
    regarding a change in the system pressures at which the fire pumps would automatically
a.  
    start (NCV 05000315-05000316/2013009-02). While the licensee was able to eventually
Inspection Scope  
    show the new setpoints were acceptable, nothing was done to explore potential
The inspectors selected a sample of previously issued NRC findings to assess the  
    breakdowns in the engineering change process or in human performance that allowed
adequacy of licensee corrective actions. Two instances were identified where the  
    the change to occur without the additional reviews being done to begin with. In another
technical issues had been adequately addressed; however, it appeared there were no  
    example, FIN 05000315-05000316/2013002-02 was issued for a failure to follow the
corrective actions for underlying performance issues. In one case, a finding was issued  
    guidance in the operability determination procedure. Subsequently, the licensee used
regarding a change in the system pressures at which the fire pumps would automatically  
    methods that were acceptable to validate the past operability of Emergency Core
start (NCV 05000315-05000316/2013009-02). While the licensee was able to eventually  
    Cooling piping when a void was discovered. However, any underlying issues in human
show the new setpoints were acceptable, nothing was done to explore potential  
    performance or in the operability determination process were not explored at the time.
breakdowns in the engineering change process or in human performance that allowed  
    The licensee acknowledged the inspectors observations.
the change to occur without the additional reviews being done to begin with. In another  
    Regarding the finding discussed above for the fire pump starting setpoints, the
example, FIN 05000315-05000316/2013002-02 was issued for a failure to follow the  
    inspectors also identified that changes had been made to the plant design basis since
guidance in the operability determination procedure. Subsequently, the licensee used  
    the licensees previous corrective actions were completed. Pursuant to the change to
methods that were acceptable to validate the past operability of Emergency Core  
    NFPA-805 standards of fire protection, additional sprinklers were added to the required
Cooling piping when a void was discovered. However, any underlying issues in human  
    Technical Requirements Manual fire suppression systems. When this occurred, the
performance or in the operability determination process were not explored at the time.
    licensee did not re-review the impacts on the fire pump starting setpoint issue which was
The licensee acknowledged the inspectors observations.  
    the subject of the NRC finding. Based on inspector questions, the licensee re-instituted
Regarding the finding discussed above for the fire pump starting setpoints, the  
    compensatory measures to restore functionality of the fire suppression system pending
inspectors also identified that changes had been made to the plant design basis since  
    approval of new calculations that will incorporate the new systems and starting setpoints
the licensees previous corrective actions were completed. Pursuant to the change to  
    of the fire pumps. Additionally, the inspectors questioned the adequacy of current fire
NFPA-805 standards of fire protection, additional sprinklers were added to the required  
    pump surveillance tests in light of the NRC finding. The inspectors discovered the
Technical Requirements Manual fire suppression systems. When this occurred, the  
                                                48
licensee did not re-review the impacts on the fire pump starting setpoint issue which was  
the subject of the NRC finding. Based on inspector questions, the licensee re-instituted  
compensatory measures to restore functionality of the fire suppression system pending  
approval of new calculations that will incorporate the new systems and starting setpoints  
of the fire pumps. Additionally, the inspectors questioned the adequacy of current fire  
pump surveillance tests in light of the NRC finding. The inspectors discovered the  


      licensee had already identified a discrepancy between the surveillance tests and design
      requirements and had written an AR in September of 2014. Basically, a pump could
49
      degrade to a point where it would still pass a surveillance, yet not meet all aspects of the
      design calculation requirements for the fire suppression system. The licensee was able
licensee had already identified a discrepancy between the surveillance tests and design  
      to demonstrate the pumps had not degraded to a point outside the design requirements,
requirements and had written an AR in September of 2014. Basically, a pump could  
      and was working to resolve the discrepancy between the tests and design requirements.
degrade to a point where it would still pass a surveillance, yet not meet all aspects of the  
      This review constituted one in-depth review of a selected issue sample as defined in
design calculation requirements for the fire suppression system. The licensee was able  
      IP 71152-05.
to demonstrate the pumps had not degraded to a point outside the design requirements,  
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)
and was working to resolve the discrepancy between the tests and design requirements.  
.1   Dual Unit Trip Caused by Debris Intrusion in the Forebay
This review constituted one in-depth review of a selected issue sample as defined in  
  a. Inspection Scope
IP 71152-05.  
      On November 1, 2014, the inspectors responded to the site following a dual unit trip
4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)  
      caused by debris intrusion in the forebay of the screenhouse. During the evening of
.1  
      October 31, and early morning of November 1, rough lake conditions and high wind
Dual Unit Trip Caused by Debris Intrusion in the Forebay
      mobilized and transported a large mass of sea grass and other debris. This debris
a.  
      entered the D.C. Cook intake structure and collected on trash racks and travelling
Inspection Scope  
      screens in the fore bay. Prior to the unit shutdown, the licensee monitored forebay
On November 1, 2014, the inspectors responded to the site following a dual unit trip  
      conditions and took actions to maintain the travelling screens clean. However, the rate
caused by debris intrusion in the forebay of the screenhouse. During the evening of  
      of debris intrusion exceeded the equipments ability to clean the screens. As differential
October 31, and early morning of November 1, rough lake conditions and high wind  
      pressure increased across the screens, the licensee entered the Degraded Forebay
mobilized and transported a large mass of sea grass and other debris. This debris  
      abnormal procedure. The licensee reduced power in Unit 2 to 50 percent and secured a
entered the D.C. Cook intake structure and collected on trash racks and travelling  
      circulating water pump. However, conditions in the fore bay continued to degrade to the
screens in the fore bay. Prior to the unit shutdown, the licensee monitored forebay  
      point that the licensee had to manually trip both units. This action allowed the licensee
conditions and took actions to maintain the travelling screens clean. However, the rate  
      to secure all circulating water pumps thus protecting the safety-related service water
of debris intrusion exceeded the equipments ability to clean the screens. As differential  
      system.
pressure increased across the screens, the licensee entered the Degraded Forebay  
      Following the plant trip, the licensee notified the resident inspector who responded to the
abnormal procedure. The licensee reduced power in Unit 2 to 50 percent and secured a  
      site. The inspectors verified licensee actions in the control rooms were consistent with
circulating water pump. However, conditions in the fore bay continued to degrade to the  
      plant procedures. In addition, the inspectors focused on performance of safety-related
point that the licensee had to manually trip both units. This action allowed the licensee  
      equipment supplied with service water. The inspectors concluded that the service water
to secure all circulating water pumps thus protecting the safety-related service water  
      system had not been impacted by the debris intrusion.
system.
      As part of the plant shutdown, several plant SSCs did not perform as expected. For
Following the plant trip, the licensee notified the resident inspector who responded to the  
      Unit 2, auto transfer between the unit auxiliary transformer and reserve auxiliary
site. The inspectors verified licensee actions in the control rooms were consistent with  
      transformer on turbine trip did not occur. Auto transfer did occur after the licensee
plant procedures. In addition, the inspectors focused on performance of safety-related  
      manually inserted a generator trip. The licensee replaced a failed relay associated with
equipment supplied with service water. The inspectors concluded that the service water  
      a turbine stop valve to correct the condition. In addition, a relay on the unit two reserve
system had not been impacted by the debris intrusion.
      auxiliary transformer failed that precluded auto-stepping of the transformer; the licensee
As part of the plant shutdown, several plant SSCs did not perform as expected. For  
      replaced this relay prior to unit startup.
Unit 2, auto transfer between the unit auxiliary transformer and reserve auxiliary  
      On Unit 1, the turbine driven auxiliary feedwater pump tripped while the licensee
transformer on turbine trip did not occur. Auto transfer did occur after the licensee  
      throttled flow. Because both MDAFW pumps were operable, the licensee used the
manually inserted a generator trip. The licensee replaced a failed relay associated with  
      MDAFW pumps for steam generator level control. The inspectors identified a finding as
a turbine stop valve to correct the condition. In addition, a relay on the unit two reserve  
      documented in Section 1R15 of this report. Additionally, on Unit 2, an AFW flow control
auxiliary transformer failed that precluded auto-stepping of the transformer; the licensee  
      valve appeared to not respond to a flow retention signal. The flow retention circuit acts
replaced this relay prior to unit startup.  
      to prevent excessive flows to the steam generators from the AFW pumps by throttling
On Unit 1, the turbine driven auxiliary feedwater pump tripped while the licensee  
                                                49
throttled flow. Because both MDAFW pumps were operable, the licensee used the  
MDAFW pumps for steam generator level control. The inspectors identified a finding as  
documented in Section 1R15 of this report. Additionally, on Unit 2, an AFW flow control  
valve appeared to not respond to a flow retention signal. The flow retention circuit acts  
to prevent excessive flows to the steam generators from the AFW pumps by throttling  


      closed flow control valves. Upon investigation, given instrument tolerances, tests of the
      circuitry, time delay settings, and actual measured flow, it was determined the system
50
      acted appropriately.
      In addition, three steam safety valves lifted prior to their nominal set point tolerance
closed flow control valves. Upon investigation, given instrument tolerances, tests of the  
      band. In reviewing the condition, the licensee documented that set point surveillances
circuitry, time delay settings, and actual measured flow, it was determined the system  
      are conducted using a defined set of conditions that allow the safeties to achieve
acted appropriately.  
      repeatable lift setpoints. For an installed safety, several factors can influence actual lift
In addition, three steam safety valves lifted prior to their nominal set point tolerance  
      pressure. These factors include vibration and temperature transients. As a result, the
band. In reviewing the condition, the licensee documented that set point surveillances  
      licensee concluded that the valves responded in a fashion consistent with the design of
are conducted using a defined set of conditions that allow the safeties to achieve  
      the valves. The licensee plans on performing lift tests on the valves during the next
repeatable lift setpoints. For an installed safety, several factors can influence actual lift  
      refueling outage to confirm valve operability.
pressure. These factors include vibration and temperature transients. As a result, the  
      This event follow-up review constituted one sample as defined in IP 71153-05.
licensee concluded that the valves responded in a fashion consistent with the design of  
  b. Findings
the valves. The licensee plans on performing lift tests on the valves during the next  
      No findings were identified.
refueling outage to confirm valve operability.
4OA6 Management Meetings
This event follow-up review constituted one sample as defined in IP 71153-05.  
.1   Exit Meeting Summary
b.  
      On January 20, 2015, the inspectors presented the inspection results to Mr. L. Weber
Findings  
      and other members of the licensee staff. The licensee acknowledged the issues
No findings were identified.  
      presented. The inspectors confirmed that none of the potential report input discussed
4OA6 Management Meetings  
      was considered proprietary.
.1  
.2   Interim Exit Meetings
Exit Meeting Summary  
      Interim exits were conducted for:
On January 20, 2015, the inspectors presented the inspection results to Mr. L. Weber  
      *       The results of the inservice inspection were discussed with site vice president,
and other members of the licensee staff. The licensee acknowledged the issues  
              Mr. J. Gebbie on October 10, 2014;
presented. The inspectors confirmed that none of the potential report input discussed  
      *       The inspection results for the areas of radiological hazard assessment and
was considered proprietary.  
              exposure controls; occupational ALARA planning and controls; and occupational
.2  
              exposure control effectiveness performance indicator verification with
Interim Exit Meetings  
              Mr. J. Gebbie, Site Vice President, on October 17, 2014;
Interim exits were conducted for:  
      *       The inspection results for the area of radiological hazard assessment and
*  
              exposure controls with Mr. J. Gebbe, Site Vice President, on October 29, 2014;
The results of the inservice inspection were discussed with site vice president,  
      *       The inspection results for the areas of radiological environmental monitoring; and
Mr. J. Gebbie on October 10, 2014;  
              RCS specific activity and RETS/ODCM radiological effluent occurrences
*  
              performance indicator verification with Mr. J. Gebbe, Site Vice President, on
The inspection results for the areas of radiological hazard assessment and  
              November 7, 2014;
exposure controls; occupational ALARA planning and controls; and occupational  
      *       The results of the inspection of the permanent removal of shield/missile blocks
exposure control effectiveness performance indicator verification with
              with Mr. L. Weber, Chief Nuclear Officer, and other members of the licensee staff
Mr. J. Gebbie, Site Vice President, on October 17, 2014;  
              on December 01, 2014; and
*  
      *       The Annual Review of Emergency Action Level and Emergency Plan Changes
The inspection results for the area of radiological hazard assessment and  
              with the Licensee's Chief Nuclear Officer, Mr. L. Weber, on January 12, 2015.
exposure controls with Mr. J. Gebbe, Site Vice President, on October 29, 2014;  
                                                50
*  
The inspection results for the areas of radiological environmental monitoring; and  
RCS specific activity and RETS/ODCM radiological effluent occurrences  
performance indicator verification with Mr. J. Gebbe, Site Vice President, on  
November 7, 2014;  
*  
The results of the inspection of the permanent removal of shield/missile blocks  
with Mr. L. Weber, Chief Nuclear Officer, and other members of the licensee staff  
on December 01, 2014; and  
*  
The Annual Review of Emergency Action Level and Emergency Plan Changes  
with the Licensee's Chief Nuclear Officer, Mr. L. Weber, on January 12, 2015.  


    The inspectors confirmed that none of the potential report input discussed was
    considered proprietary. Proprietary material received during the inspection was returned
51
    to the licensee.
ATTACHMENT: SUPPLEMENTAL INFORMATION
The inspectors confirmed that none of the potential report input discussed was  
                                            51
considered proprietary. Proprietary material received during the inspection was returned  
to the licensee.  
ATTACHMENT: SUPPLEMENTAL INFORMATION


                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee
L. Weber, Chief Nuclear Officer
Attachment
J. Gebbie, Site Vice President
SUPPLEMENTAL INFORMATION  
L. Baun, Director Performance Assurance
KEY POINTS OF CONTACT  
J. Beer, Principal Health Physicist
Licensee  
D. Bronicki, Interim Radiation Protection Manager
L. Weber, Chief Nuclear Officer  
R. Hall, ISI Program Owner
J. Gebbie, Site Vice President  
J. Harner, Environmental Manager
L. Baun, Director Performance Assurance  
G. Hill, Supervisor Nuclear Safety Analysis
J. Beer, Principal Health Physicist  
S. Lies, Vice President Engineering
D. Bronicki, Interim Radiation Protection Manager  
S. Mitchell, Regulatory Affairs
R. Hall, ISI Program Owner  
D. Miller, Health Physicist
J. Harner, Environmental Manager  
J. Nimtz, Senior Licensing Activity Coordinator
G. Hill, Supervisor Nuclear Safety Analysis  
J. Ross, Engineering Director
S. Lies, Vice President Engineering  
M. Scarpello, Regulatory Affairs Manager
S. Mitchell, Regulatory Affairs  
P. Schoepf, Nuclear Site Services Director
D. Miller, Health Physicist  
R. Sieber, Emergency Preparedness Manager
J. Nimtz, Senior Licensing Activity Coordinator  
Nuclear Regulatory Commission
J. Ross, Engineering Director  
K. Riemer, Chief, Reactor Projects Branch 2
M. Scarpello, Regulatory Affairs Manager  
R. Daley, Chief, Engineering Branch 3
P. Schoepf, Nuclear Site Services Director  
B. Dickson, Chief, Health Physics and Incident Response
R. Sieber, Emergency Preparedness Manager  
N. Feliz-Adorno, Reactor Engineer
Nuclear Regulatory Commission  
J. Gilliam; Reactor Engineer
K. Riemer, Chief, Reactor Projects Branch 2  
M. Mitchell, Health Physicist
R. Daley, Chief, Engineering Branch 3  
                                                        Attachment
B. Dickson, Chief, Health Physics and Incident Response  
N. Feliz-Adorno, Reactor Engineer  
J. Gilliam; Reactor Engineer
M. Mitchell, Health Physicist  


                LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
2
05000315/2014005-01   NCV   Failure to Identify Conditions Adverse to Quality
                            associated with the Unit 1 TDAFW Pump Turbine Oil
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED  
                            System (Section 1R15.b(1))
Opened  
05000315/2014005-02; NCV   Unplanned Inoperability of the AB Fuel Oil Storage Tank
05000315/2014005-01  
05000316/2014005-02        during Maintenance (Section 1R15.b(2))
NCV  
05000315/2014005-03; NCV   Inadequate Review of Radiological Impact of the Removal
Failure to Identify Conditions Adverse to Quality  
05000316/2014005-03        of the Auxiliary Shield Blocks on the Containment
associated with the Unit 1 TDAFW Pump Turbine Oil  
                            Accident Shield Post LBLOCA (Section 1R18)
System (Section 1R15.b(1))  
05000315/2014005-04   NCV   Inadvertent Trip of the Unit 1 TDAFW Pump
05000315/2014005-02;  
                            (Section 1R19)
05000316/2014005-02
05000315/2014005-05   URI   Changes to Minimum 60-Minute Emergency Responder
NCV  
                            Staffing Without Prior Approval (Section 1EP4)
Unplanned Inoperability of the AB Fuel Oil Storage Tank  
05000315/2014005-06; NCV   Failure To Identify Deficient Locked High Radiation Area
during Maintenance (Section 1R15.b(2))  
05000316/2014005-06        Controls Due To Procedure Inadequacy (Section 2RS1.4)
05000315/2014005-03;  
Closed
05000316/2014005-03
05000315/2014005-01   NCV   Failure to Identify Conditions Adverse to Quality
NCV  
                            associated with the Unit 1 TDAFW Pump Turbine Oil
Inadequate Review of Radiological Impact of the Removal  
                            System (Section 1R15.b(1))
of the Auxiliary Shield Blocks on the Containment  
05000315/2014005-02; NCV   Unplanned Inoperability of the AB Fuel Oil Storage Tank
Accident Shield Post LBLOCA (Section 1R18)  
05000316/2014005-02        during Maintenance (Section 1R15.b(2))
05000315/2014005-04  
05000315/2014005-03; NCV   Inadequate Review of Radiological Impact of the Removal
NCV  
05000316/2014005-03        of the Auxiliary Shield Blocks on the Containment
Inadvertent Trip of the Unit 1 TDAFW Pump  
                            Accident Shield Post LBLOCA (Section 1R18)
(Section 1R19)  
05000315/2014005-04   NCV   Inadvertent Trip of the Unit 1 TDAFW Pump
05000315/2014005-05  
                            (Section 1R19)
URI  
05000315/2014005-06; NCV   Failure To Identify Deficient Locked High Radiation Area
Changes to Minimum 60-Minute Emergency Responder  
05000316/2014005-06        Controls Due To Procedure Inadequacy (Section 2RS1.4)
Staffing Without Prior Approval (Section 1EP4)  
Discussed
05000315/2014005-06;  
None
05000316/2014005-06
                                        2
NCV  
Failure To Identify Deficient Locked High Radiation Area  
Controls Due To Procedure Inadequacy (Section 2RS1.4)  
Closed  
05000315/2014005-01  
NCV  
Failure to Identify Conditions Adverse to Quality  
associated with the Unit 1 TDAFW Pump Turbine Oil  
System (Section 1R15.b(1))  
05000315/2014005-02;  
05000316/2014005-02
NCV  
Unplanned Inoperability of the AB Fuel Oil Storage Tank  
during Maintenance (Section 1R15.b(2))  
05000315/2014005-03;  
05000316/2014005-03
NCV  
Inadequate Review of Radiological Impact of the Removal  
of the Auxiliary Shield Blocks on the Containment  
Accident Shield Post LBLOCA (Section 1R18)  
05000315/2014005-04  
NCV  
Inadvertent Trip of the Unit 1 TDAFW Pump  
(Section 1R19)  
05000315/2014005-06;  
05000316/2014005-06
NCV  
Failure To Identify Deficient Locked High Radiation Area  
Controls Due To Procedure Inadequacy (Section 2RS1.4)  
Discussed  
None  


                                  LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
3
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
selected sections or portions of the documents were evaluated as part of the overall inspection
LIST OF DOCUMENTS REVIEWED  
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
The following is a partial list of documents reviewed during the inspection. Inclusion on this list  
any part of it, unless this is stated in the body of the inspection report.
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that  
1R01 Adverse Weather Protection
selected sections or portions of the documents were evaluated as part of the overall inspection  
- 12-IHP-5040-EMP-004, Plant Winterization and De-Winterization, Revision 21
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7
any part of it, unless this is stated in the body of the inspection report.  
- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22
1R01 Adverse Weather Protection  
- AR-2014-14403, 12-HV-DGH Appears to Have Failed
- 12-IHP-5040-EMP-004, Plant Winterization and De-Winterization, Revision 21  
- Cook Seasonal Readiness Affirmation Letter, November 11, 2014
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7  
- PMP-5055-001-001, Winterization/Summerization Checklist, Revision 22
- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22  
1R04 Equipment Alignment
- AR-2014-14403, 12-HV-DGH Appears to Have Failed  
- 2-OHP-4021-017-002, Placing in Service the Residual Heat Removal System, Revision 24
- Cook Seasonal Readiness Affirmation Letter, November 11, 2014  
- 2-OHP-4030-217-050W, West Residual Heat Removal Train Operability Test, Modes 1-4,
- PMP-5055-001-001, Winterization/Summerization Checklist, Revision 22  
  Revision 14
1R04 Equipment Alignment  
- AR-2014-14089, CTS Nozzle Leaking
- 2-OHP-4021-017-002, Placing in Service the Residual Heat Removal System, Revision 24  
- AR-2014-8502, Possible PORV Leakby
- 2-OHP-4030-217-050W, West Residual Heat Removal Train Operability Test, Modes 1-4,  
- Drawing OP-1-5144-51, Containment Spray
Revision 14  
- Drawing OP-2-5105D-22, Steam Generating System
- AR-2014-14089, CTS Nozzle Leaking  
- Drawing OP-2-5106A-55, Aux Feedwater
- AR-2014-8502, Possible PORV Leakby  
- List of Open Work Orders, Unit 1 Containment Spray System
- Drawing OP-1-5144-51, Containment Spray  
1R05 Fire Protection
- Drawing OP-2-5105D-22, Steam Generating System  
- AR 2014-15683, Combustible Material Stored in 2AB DB FO Transfer Pump Room
- Drawing OP-2-5106A-55, Aux Feedwater  
- AR-2014-12540, Unattended Test Equipment
- List of Open Work Orders, Unit 1 Containment Spray System  
- CNP Fire Safety Analysis, Report R1900-007-AA32, Fire Area 32, June 2011
1R05 Fire Protection  
- Fire Hazards Analysis, Revision 16
- AR 2014-15683, Combustible Material Stored in 2AB DB FO Transfer Pump Room  
- PMP-2270-CCM-001, Control of Combustible Materials, Revision 24
- AR-2014-12540, Unattended Test Equipment  
- PMP-2270-WBG-001, Welding, Burning, and Grinding Activities, Revision 23
- CNP Fire Safety Analysis, Report R1900-007-AA32, Fire Area 32, June 2011  
1R06 Flooding
- Fire Hazards Analysis, Revision 16  
- 12-1141-53, 34.5Kv & 4 Kv Power Duct Runs & Control Cable Pipe Runs in Plant Yard Area,
- PMP-2270-CCM-001, Control of Combustible Materials, Revision 24  
  April 4, 1971
- PMP-2270-WBG-001, Welding, Burning, and Grinding Activities, Revision 23  
1R07 Heat Sink Performance
1R06 Flooding  
- 12-EHP-8913-001-002, Heat Exchanger Inspection, Revision 9
- 12-1141-53, 34.5Kv & 4 Kv Power Duct Runs & Control Cable Pipe Runs in Plant Yard Area,  
- D.C. Cook Commitment Change Number CC-0218, Regarding Heat Exchanger Inspection
April 4, 1971  
  Program, March 10, 2003
1R07 Heat Sink Performance  
- Fall 2014 U1C26 Eddy Current Inspection Results, 1-HE-47-CDN Heat Exchanger
- 12-EHP-8913-001-002, Heat Exchanger Inspection, Revision 9  
- NRC Generic Letter 89-13, Service Water System Problems Affecting Safety-Related
- D.C. Cook Commitment Change Number CC-0218, Regarding Heat Exchanger Inspection  
  Equipment, July 18, 1989
Program, March 10, 2003  
                                                    3
- Fall 2014 U1C26 Eddy Current Inspection Results, 1-HE-47-CDN Heat Exchanger  
- NRC Generic Letter 89-13, Service Water System Problems Affecting Safety-Related  
Equipment, July 18, 1989  


1R08 Inservice Inspection Activities
- 12-EHP-5037-SGP-004, Steam Generator Foreign Object Disposition, Revision 5
4
- 12-EHP-5070-NDE-DMW, Ultrasonic Examination of ASME Section XI, Appendix VIII,
  Supplement 10 Dissimilar Metal Welds, Revision 0
1R08 Inservice Inspection Activities  
- 12-QHP-5050-NDE-002, Magnetic Particle Examination, Revision 6
- 12-EHP-5037-SGP-004, Steam Generator Foreign Object Disposition, Revision 5  
- 12-QHP-5050-NDE-010, Radiographic Examination of Welds, Revision 6
- 12-EHP-5070-NDE-DMW, Ultrasonic Examination of ASME Section XI, Appendix VIII,  
- 1-EHP-4030-102-001, Steam Generator Primary Side Surveillance, Revision 10
Supplement 10 Dissimilar Metal Welds, Revision 0  
- AR 2012-12105, Water Pooling Around U2 CST
- 12-QHP-5050-NDE-002, Magnetic Particle Examination, Revision 6  
- AR 2013-0534, 12-CS-185 has a Body to Bonnet Leak
- 12-QHP-5050-NDE-010, Radiographic Examination of Welds, Revision 6  
- AR 2013-4317, 1-QRV-114, Body to Bonnet Leak
- 1-EHP-4030-102-001, Steam Generator Primary Side Surveillance, Revision 10  
- AR 2013-4625, 1-CS-448-1 has a BA Leak
- AR 2012-12105, Water Pooling Around U2 CST  
- AR 2013-5096, No. 14 SG Cold Leg Nozzle Dam Leakage
- AR 2013-0534, 12-CS-185 has a Body to Bonnet Leak  
- AR 2013-5279, 12-QLA-420-IDH BA Leak from Swedgelock Fitting
- AR 2013-4317, 1-QRV-114, Body to Bonnet Leak  
- AR 2013-6540, 1-SF-160 Leaking at Diaphragm
- AR 2013-4625, 1-CS-448-1 has a BA Leak  
- AR 2013-6839, U1C25 Refueling Cavity Leakage
- AR 2013-5096, No. 14 SG Cold Leg Nozzle Dam Leakage  
- AR 2013-7061, 1-RH-147W has Boric Acic on Body to Bonnet
- AR 2013-5279, 12-QLA-420-IDH BA Leak from Swedgelock Fitting  
- AR 2013-7067, 1-RH-107W Leaks by at 0.095 ml/min
- AR 2013-6540, 1-SF-160 Leaking at Diaphragm  
- AR 2013-7220, Reactor Head and Pressurizer Vent Piping Areas
- AR 2013-6839, U1C25 Refueling Cavity Leakage  
- AR 2013-7354, Evidence of Previous Small Boric Acid Leak from 1-NFP-211
- AR 2013-7061, 1-RH-147W has Boric Acic on Body to Bonnet  
- AR 2013-7355, 1-NFP-240 has Evidence of Prior Test Fitting Leakage
- AR 2013-7067, 1-RH-107W Leaks by at 0.095 ml/min  
- AR 2013-8587, U1 Seal Table Thimble Leakage Identified
- AR 2013-7220, Reactor Head and Pressurizer Vent Piping Areas  
- AR 2013-9459, 12-CS-185 has a Ruptured Diaphragm
- AR 2013-7354, Evidence of Previous Small Boric Acid Leak from 1-NFP-211  
- AR 2014-8869, 1-QRV-200, Active Boric Acid Leak on Packing
- AR 2013-7355, 1-NFP-240 has Evidence of Prior Test Fitting Leakage  
- AR 2014-11337, Wall Loss Identified in NESW Containment Penetration Piping
- AR 2013-8587, U1 Seal Table Thimble Leakage Identified  
- AR 2014-11339, Piping Wall Loss Near 1-WCR-942
- AR 2013-9459, 12-CS-185 has a Ruptured Diaphragm  
- AR 2014-11413, Six Data Points In Piping Found Below Manufact Tolerance
- AR 2014-8869, 1-QRV-200, Active Boric Acid Leak on Packing  
- AR 2014-11518, Six Data Points In Piping Found Below Design Minimum
- AR 2014-11337, Wall Loss Identified in NESW Containment Penetration Piping  
- AR 2014-11519, Two Data Points In Piping Found Below Design Minimum
- AR 2014-11339, Piping Wall Loss Near 1-WCR-942  
- AR 2014-11664, NESW Pipe Wall Below Manufacturers Tolerance
- AR 2014-11413, Six Data Points In Piping Found Below Manufact Tolerance  
- AR 2014-12108, NRC Observation: Boric Acid not Included in GE I-8000
- AR 2014-11518, Six Data Points In Piping Found Below Design Minimum  
- AR 2014-12160, Technician Understanding of Range of Coverage Questioned
- AR 2014-11519, Two Data Points In Piping Found Below Design Minimum  
- AR 2014-12162, NRC Inservice Inspection Observation
- AR 2014-11664, NESW Pipe Wall Below Manufacturers Tolerance  
- AR 2014-1218, AR for Boric Acid Leak Not Properly Screened
- AR 2014-12108, NRC Observation: Boric Acid not Included in GE I-8000  
- AR 2014-12384, NRC Observation During U1 Inservice Inspection
- AR 2014-12160, Technician Understanding of Range of Coverage Questioned  
- AR 2014-3762, Previously Identified BA Leak on 1-SI-128
- AR 2014-12162, NRC Inservice Inspection Observation  
- DIT-B-03569-01, AEP Design Information Transmittal, October 7, 2014
- AR 2014-1218, AR for Boric Acid Leak Not Properly Screened  
- ETSS No. 1, Bobbin Coil, Revision 0
- AR 2014-12384, NRC Observation During U1 Inservice Inspection  
- ETSS No. 2, 3 Coil MRPC, Revision 0
- AR 2014-3762, Previously Identified BA Leak on 1-SI-128  
- LMT-04-UT-012, Manual Phased Array Ultrasonic Examination of Weld Overlaid Similar and
- DIT-B-03569-01, AEP Design Information Transmittal, October 7, 2014  
  Dissimilar Metal Welds, Revision 0
- ETSS No. 1, Bobbin Coil, Revision 0  
- LMT-04-UT-113, Ultrasonic Examination of Nozzle Inner Radius Areas, Revision 7
- ETSS No. 2, 3 Coil MRPC, Revision 0  
- LMT-10-PAUT-002, Manual Phased Array Ultrasonic Examination of Austenitic and Ferritic
- LMT-04-UT-012, Manual Phased Array Ultrasonic Examination of Weld Overlaid Similar and  
  Piping Welds, Revision 0
Dissimilar Metal Welds, Revision 0  
- PDI-UT-11, Generic Procedure for the Ultrasonic Detection and Sizing of Reactor Pressure
- LMT-04-UT-113, Ultrasonic Examination of Nozzle Inner Radius Areas, Revision 7  
  Vessel Nozzle-to-Shell Welds and Nozzle Inner Radius, Revision C
- LMT-10-PAUT-002, Manual Phased Array Ultrasonic Examination of Austenitic and Ferritic  
- PMI-5070, Inservice Inspection, Revision 21
Piping Welds, Revision 0  
- PMP-5030-001-001, Boric Acid Corrosion Control, Revision 17
- PDI-UT-11, Generic Procedure for the Ultrasonic Detection and Sizing of Reactor Pressure  
- PQR 136, ASME Procedure Qualification Record, Revision 1
Vessel Nozzle-to-Shell Welds and Nozzle Inner Radius, Revision C  
- PQR 219, ASME Procedure Qualification Record, Revision 1
- PMI-5070, Inservice Inspection, Revision 21  
- PQR 256, ASME Procedure Qualification Record, Revision 1
- PMP-5030-001-001, Boric Acid Corrosion Control, Revision 17  
                                              4
- PQR 136, ASME Procedure Qualification Record, Revision 1  
- PQR 219, ASME Procedure Qualification Record, Revision 1  
- PQR 256, ASME Procedure Qualification Record, Revision 1  


- PQR 258, ASME Procedure Qualification Record, Revision 1
- QA-46, Qualification and Certification NDE and Visual Examination Personnel, Revision 3
5
- S000126-AST-000001, Steam Generator Degradation Assessment, Revision 0
- S000126-WKI-000020, D.C. Cook Unit 1 Steam Generator Eddy Current Testing Site
- PQR 258, ASME Procedure Qualification Record, Revision 1  
  Technique Validation, Revision 0
- QA-46, Qualification and Certification NDE and Visual Examination Personnel, Revision 3  
- U1-MT-14-001, Magnetic Particle Examination, October 4, 2014
- S000126-AST-000001, Steam Generator Degradation Assessment, Revision 0  
- U1-PT-14-004, Liquid Penetrant Examination, October 2, 2014
- S000126-WKI-000020, D.C. Cook Unit 1 Steam Generator Eddy Current Testing Site  
- U1-PT-14-005, Liquid Penetrant Examination, October 2, 2014
Technique Validation, Revision 0  
- U1-VE-14-003, Ultrasonic Examination, October 2, 2014
- U1-MT-14-001, Magnetic Particle Examination, October 4, 2014  
- U1-VE-14-004, Ultrasonic Examination, October 2, 2014
- U1-PT-14-004, Liquid Penetrant Examination, October 2, 2014  
- U1-VE-14-014, Ultrasonic Examination, October 8, 2014
- U1-PT-14-005, Liquid Penetrant Examination, October 2, 2014  
- UT-110, Ultrasonic Examination of Vessel Welds and Adjacent Base Metal >2.0 in Thickness,
- U1-VE-14-003, Ultrasonic Examination, October 2, 2014  
  Revision 2
- U1-VE-14-004, Ultrasonic Examination, October 2, 2014  
- WO 55390312-01, Replacement of 1-NLI-112-V1, October 7, 2014
- U1-VE-14-014, Ultrasonic Examination, October 8, 2014  
- WO 55392571-01, Replacement of 1-NRV-102, March 12, 2013
- UT-110, Ultrasonic Examination of Vessel Welds and Adjacent Base Metal >2.0 in Thickness,  
- WO 55404504-06, EC 52036, Install New Snubber Pipe Support 1-ARC-S-4012,
Revision 2  
  March 8, 2013
- WO 55390312-01, Replacement of 1-NLI-112-V1, October 7, 2014  
- WO 55421212-10/13, Replacement of 1-NFP-222-V2, March 6, 2013
- WO 55392571-01, Replacement of 1-NRV-102, March 12, 2013  
- WO 55440759-05, Install Valve Assembly 1-CS-314, October 7, 2014z
- WO 55404504-06, EC 52036, Install New Snubber Pipe Support 1-ARC-S-4012,  
- WPS 8.12T, Welding Procedure Specification, Revision 1
March 8, 2013  
- WPS 8.1TS, Welding Procedure Specification, Revision 4
- WO 55421212-10/13, Replacement of 1-NFP-222-V2, March 6, 2013  
1R11 Licensed Operator Requilification Program
- WO 55440759-05, Install Valve Assembly 1-CS-314, October 7, 2014z  
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25
- WPS 8.12T, Welding Procedure Specification, Revision 1  
- November 19, 2014, Training Exercise Guide and Drill Guide
- WPS 8.1TS, Welding Procedure Specification, Revision 4  
- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4
1R11 Licensed Operator Requilification Program  
1R12 Maintenance Effectiveness
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25  
- 1-IHP-6030-IMP-002, NARPI System Operational Test and Linearization, Revision 11
- November 19, 2014, Training Exercise Guide and Drill Guide  
- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11
- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4  
- 2012-2013 AMSAC, Unavailability Hours Reports
- AR 2010-10345, U2 Letdown Isolation after Shutdown Due to RCS Cooldown
1R12 Maintenance Effectiveness  
- AR 2012-14344, 2-URV-125 Failed To Stroke Fully Open
- 1-IHP-6030-IMP-002, NARPI System Operational Test and Linearization, Revision 11  
- AR 2012-14364-1, 1-NRI-16 Found Out of Spec
- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11  
- AR 2012-16048, 1-URV-125 Failed Drop Test
- 2012-2013 AMSAC, Unavailability Hours Reports  
- AR 2012-4275, Steam Dump System Operation
- AR 2010-10345, U2 Letdown Isolation after Shutdown Due to RCS Cooldown  
- AR 2013-10252, 1-URV-136 Failed Drop Test
- AR 2012-14344, 2-URV-125 Failed To Stroke Fully Open  
- AR 2013-1157, 1-NRI-50 Lower Section Power Supply Out of Tolerance
- AR 2012-14364-1, 1-NRI-16 Found Out of Spec  
- AR 2013-1164, 2-MRV-212 Failed Stroke Time
- AR 2012-16048, 1-URV-125 Failed Drop Test  
- AR 2013-11973, Unit 2 MS-02 has Exceeded its Unavailability Limit
- AR 2012-4275, Steam Dump System Operation  
- AR 2013-3420, Flux Differential Indicators Found Out of Tolerance
- AR 2013-10252, 1-URV-136 Failed Drop Test  
- AR 2013-4315, 1-MRV-231 Fail to Close Upon Return to Neutral
- AR 2013-1157, 1-NRI-50 Lower Section Power Supply Out of Tolerance  
- AR 2013-4320, 1-URV-110 Failing to Open
- AR 2013-1164, 2-MRV-212 Failed Stroke Time  
- AR 2013-4349, 1-URV-112 Failed to Open When Required
- AR 2013-11973, Unit 2 MS-02 has Exceeded its Unavailability Limit  
- AR 2013-4373-1, U-1 Scaler/Timer did Not Have Audible Counts Following S/D
- AR 2013-3420, Flux Differential Indicators Found Out of Tolerance  
- AR 2013-5060, 1-URV-111 Would not Stroke During Testing
- AR 2013-4315, 1-MRV-231 Fail to Close Upon Return to Neutral  
- AR 2013-6243, 2-MRV-212 Failed IST Stroke Times
- AR 2013-4320, 1-URV-110 Failing to Open  
- AR 2013-8216, 2-NRI-44B +25V Power Supply Degraded
- AR 2013-4349, 1-URV-112 Failed to Open When Required  
- AR 2014-0045, 2-URV-120 Failed Drop Test
- AR 2013-4373-1, U-1 Scaler/Timer did Not Have Audible Counts Following S/D  
                                                5
- AR 2013-5060, 1-URV-111 Would not Stroke During Testing  
- AR 2013-6243, 2-MRV-212 Failed IST Stroke Times  
- AR 2013-8216, 2-NRI-44B +25V Power Supply Degraded  
- AR 2014-0045, 2-URV-120 Failed Drop Test  


- AR 2014-11324, Steam Dumps Did Not Operate Per Procedure
- AR 2014-11739, Critical Parameter Found Out of Tolerance
6
- AR 2014-12621, 1-URV-112 Drop Test Failed
- AR 2014-13085, 1-URV-112 Has Been Failed for a Complete Cycle
- AR 2014-11324, Steam Dumps Did Not Operate Per Procedure  
- AR 2014-13088, Failure to Perform MRE on 1-URV-112 in U1C25
- AR 2014-11739, Critical Parameter Found Out of Tolerance  
- AR 2014-13277, Unit 1 Main Steam Function MS-09 (a)(1) Process
- AR 2014-12621, 1-URV-112 Drop Test Failed  
- AR 2014-14971, Unit 2 Main Steam Function MS-05 (a)(1) Process
- AR 2014-13085, 1-URV-112 Has Been Failed for a Complete Cycle  
- AR 2014-15004, As Found Data Out of Tolerance
- AR 2014-13088, Failure to Perform MRE on 1-URV-112 in U1C25  
- AR 2014-15113, ACE and MRE in AR 2013-6243 Are Not In Agreement
- AR 2014-13277, Unit 1 Main Steam Function MS-09 (a)(1) Process  
- AR 2014-2686, 1-MRV-232 Exceeded Max Stroke Time Limit During PMT
- AR 2014-14971, Unit 2 Main Steam Function MS-05 (a)(1) Process  
- AR 2014-2719, 1-MRV-232 SG #3 Stop Valve Dump Valve
- AR 2014-15004, As Found Data Out of Tolerance  
- AR-2013-10084, B6 Rod IRPI Lost During Maintenance, July 13, 2013
- AR 2014-15113, ACE and MRE in AR 2013-6243 Are Not In Agreement  
- AR-2013-12121, RPI Failure Rod D8, August 19, 2013
- AR 2014-2686, 1-MRV-232 Exceeded Max Stroke Time Limit During PMT  
- AR-2013-19212, Unit 1 RPI for B6 Inoperable, December 17, 2013
- AR 2014-2719, 1-MRV-232 SG #3 Stop Valve Dump Valve  
- AR-2013-7039, 1-RPIS-M8-SC New Module Faulty, May 10, 2013
- AR-2013-10084, B6 Rod IRPI Lost During Maintenance, July 13, 2013  
- AR-2013-7366, During Test Rod C7 Stayed at 0, May 17, 2013
- AR-2013-12121, RPI Failure Rod D8, August 19, 2013  
- AR-2013-768, Control Bank D F-14 Rod Outside and, May 25, 2013
- AR-2013-19212, Unit 1 RPI for B6 Inoperable, December 17, 2013  
- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,
- AR-2013-7039, 1-RPIS-M8-SC New Module Faulty, May 10, 2013  
  October 23, 2014
- AR-2013-7366, During Test Rod C7 Stayed at 0, May 17, 2013  
- ATWS Mitigation Actuation System (AMSAC) Maintenance Rule Scoping Document,
- AR-2013-768, Control Bank D F-14 Rod Outside and, May 25, 2013  
  Revision 1
- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,  
- GT 2013-11467, U2 MS Maintenance Rule Action Tracking
October 23, 2014  
- GT 2013-11615, 2013 Main Steam System Vulnerability Review
- ATWS Mitigation Actuation System (AMSAC) Maintenance Rule Scoping Document,  
- Maintenance Rule Scoping Document, AMSAC System, Revision 1
Revision 1  
- Maintenance Rule Scoping Document, Control Rod Drive, Revision 3
- GT 2013-11467, U2 MS Maintenance Rule Action Tracking  
- Maintenance Rule Scoping Document, Main Steam System, Revision 3
- GT 2013-11615, 2013 Main Steam System Vulnerability Review  
- Plant Health Committee Top Ten Equipment Issues, November 19, 2014
- Maintenance Rule Scoping Document, AMSAC System, Revision 1  
- System Health Report, Main Steam, Unit 1 and Unit 2, 3rd Quarter 2014
- Maintenance Rule Scoping Document, Control Rod Drive, Revision 3  
- Topical Report WCAP-7571, Rod Position Monitoring
- Maintenance Rule Scoping Document, Main Steam System, Revision 3  
- Two Year Unavailability Report, Main Steam System, Unit 1 and Unit 2, December 2, 2014
- Plant Health Committee Top Ten Equipment Issues, November 19, 2014  
- Various 2012-2013 AMSAC System Health Reports
- System Health Report, Main Steam, Unit 1 and Unit 2, 3rd Quarter 2014  
- Various Operator Logs, October-November 2014
- Topical Report WCAP-7571, Rod Position Monitoring  
- Various System Health Reports, AMSAC
- Two Year Unavailability Report, Main Steam System, Unit 1 and Unit 2, December 2, 2014  
1R13 Maintenance Risk Assessments and Emergent Work Control
- Various 2012-2013 AMSAC System Health Reports  
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7
- Various Operator Logs, October-November 2014  
- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22
- Various System Health Reports, AMSAC  
- 2-OHP-4030-219-022FV, ESW Flow Verification, Revision 18
1R13 Maintenance Risk Assessments and Emergent Work Control  
- AR-2014-14921, 2-HV-AFP-EAC, ESW Leak
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7  
- AR-2014-14921, 2-HV-AFP-EAC, Middle Contactor Welded Shut
- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22  
- AR-2014-14956, U2 West ESW Train INOP Due to Clearance Restoration
- 2-OHP-4030-219-022FV, ESW Flow Verification, Revision 18  
- Drawing 2-OP-5113-83, Essential Service Water
- AR-2014-14921, 2-HV-AFP-EAC, ESW Leak  
- I&C Information Change Package, ICP-00677, ESW Temperature Switches for AFW Room
- AR-2014-14921, 2-HV-AFP-EAC, Middle Contactor Welded Shut  
  Coolers, October 23, 2000
- AR-2014-14956, U2 West ESW Train INOP Due to Clearance Restoration  
- Operating Logs, Week of November 30, 2014
- Drawing 2-OP-5113-83, Essential Service Water  
- Part 1 Risk Assessments, Week of November 30, 2014
- I&C Information Change Package, ICP-00677, ESW Temperature Switches for AFW Room  
- PMP-2291-OLR-001, Online Risk Management, Revision 30
Coolers, October 23, 2000  
- Temporary Modification 2-TM-14-81, AFW Room Coolers
- Operating Logs, Week of November 30, 2014  
- WO 55457007-07, Install 2-TM-14-81
- Part 1 Risk Assessments, Week of November 30, 2014  
- WO 55457007-08, 2-HV-AFP-EAC, Perform Leak Inspection
- PMP-2291-OLR-001, Online Risk Management, Revision 30  
                                              6
- Temporary Modification 2-TM-14-81, AFW Room Coolers  
- WO 55457007-07, Install 2-TM-14-81  
- WO 55457007-08, 2-HV-AFP-EAC, Perform Leak Inspection  


1R15 Operability Determinations
- 12-EHP-5074-MOV-001, Motor Operated Valve Program, Revision 13
7
- 1-DCP-4894, Design Change Package for Standby Readiness Position of TDAFW Valves,
  November 13, 2000- Branch Technical Position ASB 10-1, Design Guidelines for AFW System
1R15 Operability Determinations  
  Pump Drive and Power Supply Diversity for PWR Plants, July 1981, Revision 2
- 12-EHP-5074-MOV-001, Motor Operated Valve Program, Revision 13  
- AR 2014-13700, Unit 1 Main Steam Safety Lifted During Plant Shutdown
- 1-DCP-4894, Design Change Package for Standby Readiness Position of TDAFW Valves,  
- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed
November 13, 2000- Branch Technical Position ASB 10-1, Design Guidelines for AFW System  
- AR-2014-14065, 2-FMO-222 leaks by 1%/hr, November 8, 2014
Pump Drive and Power Supply Diversity for PWR Plants, July 1981, Revision 2  
- AR-2014-7259, Question from NRC Sr. Resident still not Resolved
- AR 2014-13700, Unit 1 Main Steam Safety Lifted During Plant Shutdown  
- AR-2014-9877 Root Cause, AB Fuel Storage Tank Alarms
- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed  
- DB-12-AFWS, Auxiliary Feedwater System, Revision 5
- AR-2014-14065, 2-FMO-222 leaks by 1%/hr, November 8, 2014  
- Draft Safety Evaluation for ICUG-001 Revision 0, NRC, May 6, 2003
- AR-2014-7259, Question from NRC Sr. Resident still not Resolved  
- Drawing E-8708, 765kV Schematic, Revision 5
- AR-2014-9877 Root Cause, AB Fuel Storage Tank Alarms  
- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram
- DB-12-AFWS, Auxiliary Feedwater System, Revision 5  
- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram
- Draft Safety Evaluation for ICUG-001 Revision 0, NRC, May 6, 2003  
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram
- Drawing E-8708, 765kV Schematic, Revision 5  
- EC-53931, Revise Unit 1 Ice Basket Weight Acceptance Criteria for Unit 1 Cycle 26
- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram  
- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25
- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram  
- FSAR Section 8.0, Electrical Systems, Revision 25
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram  
- FSAR Section 8.3, Station Service Systems, Revision 25
- EC-53931, Revise Unit 1 Ice Basket Weight Acceptance Criteria for Unit 1 Cycle 26  
- Ice Condenser Utility Group Topical Report ICUG-001, Revision 3, October 23, 2003
- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25  
- NRC Letter to all Operating Plants, Discussion of TMI Lessons-Learned, October 30, 1979
- FSAR Section 8.0, Electrical Systems, Revision 25  
1R18 Plant Modifications
- FSAR Section 8.3, Station Service Systems, Revision 25  
- AR 2014-13016, Accident Shield Requirements
- Ice Condenser Utility Group Topical Report ICUG-001, Revision 3, October 23, 2003  
- Calculation Number RS-C-0046, Doses and Dose Rates from Post LOCA Airborne Sources,
- NRC Letter to all Operating Plants, Discussion of TMI Lessons-Learned, October 30, 1979  
  Revision 06
1R18 Plant Modifications  
- Calculation Number RS-C-0171, Time Dependent Post LOCA Area by Dose Rates,
- AR 2014-13016, Accident Shield Requirements  
  Revision 03
- Calculation Number RS-C-0046, Doses and Dose Rates from Post LOCA Airborne Sources,  
- Calculation Number RS-C-0232, Equipment Hatch Dose Rates - Gap Release, Revision 01
Revision 06  
- D.C. Cook, Updated Final Safety Analysis Report (UFSAR), Several Revisions Including
- Calculation Number RS-C-0171, Time Dependent Post LOCA Area by Dose Rates,  
  Revision 23
Revision 03  
- Engineering Calculation EC-0000049191, Units 1 and 2 Auxiliary Missile Block Removal
- Calculation Number RS-C-0232, Equipment Hatch Dose Rates - Gap Release, Revision 01  
  Project, Revision 00
- D.C. Cook, Updated Final Safety Analysis Report (UFSAR), Several Revisions Including  
- NUREG/CR-6545, Probabilistic Accident Consequences Uncertainty Analysis, Volume 2
Revision 23  
- PMI-601, Radiation Protection Plan, Revision 20
- Engineering Calculation EC-0000049191, Units 1 and 2 Auxiliary Missile Block Removal  
- PNNL-14424, Health Impacts from Acute Radiation Exposure, September 2003
Project, Revision 00  
- PRA-DOSE-CSSEAH, Radiation Protection for Concrete Shadow Shield for Equipment
- NUREG/CR-6545, Probabilistic Accident Consequences Uncertainty Analysis, Volume 2  
  Access Hatch, Revision 00
- PMI-601, Radiation Protection Plan, Revision 20  
1R19 Post-Maintenance Testing
- PNNL-14424, Health Impacts from Acute Radiation Exposure, September 2003  
- 12-IHP-6030-032-001, EDG Voltage Regulator Tuning and Adjustment, Revision 7
- PRA-DOSE-CSSEAH, Radiation Protection for Concrete Shadow Shield for Equipment  
- 12-IHP-6030-IMP-063, CRID Static Inverter Transfer and Auto Retransfer Tests, Revision 8
Access Hatch, Revision 00  
- 12-IHP-6030-IMP-355, Check of CRID Power Supplies, Revision 9
1R19 Post-Maintenance Testing  
- 12-MHP-5021-056-008, TDAFW Pump Governor Valve Maintenance, Revision 11
- 12-IHP-6030-032-001, EDG Voltage Regulator Tuning and Adjustment, Revision 7  
- 12-MHP-5021-056-011, Auxiliary Feedwater Pump Turbine Governor Maintenance, Revision 8
- 12-IHP-6030-IMP-063, CRID Static Inverter Transfer and Auto Retransfer Tests, Revision 8  
- 1CD EDG Aftercooler Test, 12-MHP-5021-032-015, Revision 9
- 12-IHP-6030-IMP-355, Check of CRID Power Supplies, Revision 9  
- 1-OHP-4021-056-002, Auxiliary Feed Pump Operation, Revision 32
- 12-MHP-5021-056-008, TDAFW Pump Governor Valve Maintenance, Revision 11  
                                                7
- 12-MHP-5021-056-011, Auxiliary Feedwater Pump Turbine Governor Maintenance, Revision 8  
- 1CD EDG Aftercooler Test, 12-MHP-5021-032-015, Revision 9  
- 1-OHP-4021-056-002, Auxiliary Feed Pump Operation, Revision 32  


- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24
8
- 1-OHP-4024-119, Drop 29 Alarm, CRID 3 Inverter Abnormal Actions, Revision 34
- 1-OHP-4030-156-017R, AFW Pump Response Time, Revision 3
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24  
- 1-OHP-4030-156-017T, TDAFW System Test, Revision 16
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24  
- 2-EHP-6040-256-126, U2 FMO Intermediate Position High Flow Signal Test, Revision 1
- 1-OHP-4024-119, Drop 29 Alarm, CRID 3 Inverter Abnormal Actions, Revision 34  
- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed
- 1-OHP-4030-156-017R, AFW Pump Response Time, Revision 3  
- AR-2014-13724, 2-FMO-242 Went Full Open During Unit 2 Trip
- 1-OHP-4030-156-017T, TDAFW System Test, Revision 16  
- AR-2014-13730, U1 TDAFW Sentinel Valve Lifted
- 2-EHP-6040-256-126, U2 FMO Intermediate Position High Flow Signal Test, Revision 1  
- AR-2014-14188, Failure in Synch Circuit for 2A7
- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed  
- DB-12-AFWS, Auxiliary Feedwater System, Revision 5
- AR-2014-13724, 2-FMO-242 Went Full Open During Unit 2 Trip  
- Drawing 1-OP-5106A-61, Auxiliary Feedwater
- AR-2014-13730, U1 TDAFW Sentinel Valve Lifted  
- Drawing E-8708, 765kV Schematic, Revision 5
- AR-2014-14188, Failure in Synch Circuit for 2A7  
- Drawing OP-2-5106A-55, Auxiliary Feedwater
- DB-12-AFWS, Auxiliary Feedwater System, Revision 5  
- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram
- Drawing 1-OP-5106A-61, Auxiliary Feedwater  
- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram
- Drawing E-8708, 765kV Schematic, Revision 5  
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram
- Drawing OP-2-5106A-55, Auxiliary Feedwater  
- EPRI Technical Report, Guidelines for Technical Evaluation of Replacement Items in Nuclear
- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram  
  Power Plants (NCIG-11)
- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram  
- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25
- Drawing OP-2-98101-34, Turbine Control Elementary Diagram  
- FSAR Section 8.0, Electrical Systems, Revision 25
- EPRI Technical Report, Guidelines for Technical Evaluation of Replacement Items in Nuclear  
- FSAR Section 8.3, Station Service Systems, Revision 25
Power Plants (NCIG-11)  
- Gasket Technical Data Sheets for 1CD EDG Aftercooler
- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25  
- IN-86-14, PWR Auxiliary Feedwater Pump Control Problems
- FSAR Section 8.0, Electrical Systems, Revision 25  
- IN-93-51, Repetitive Overspeed Tripping of TDAFW pumps
- FSAR Section 8.3, Station Service Systems, Revision 25  
- Plant Computer Printouts, AFW system, November 1, 2014
- Gasket Technical Data Sheets for 1CD EDG Aftercooler  
- PMP-2291-PMT-001, Work Management Post-Maintenance Testing Matrices, Revision 25
- IN-86-14, PWR Auxiliary Feedwater Pump Control Problems  
- Scheduled Work, 1AB EDG, Unit 1 Fall 2014 Refueling Outage
- IN-93-51, Repetitive Overspeed Tripping of TDAFW pumps  
- Terry Turbine Vendor Manual
- Plant Computer Printouts, AFW system, November 1, 2014  
- WO 55425039-15, Investigate Governor Valve
- PMP-2291-PMT-001, Work Management Post-Maintenance Testing Matrices, Revision 25  
- WO 55432038-01, Replace 1-CRID-3-INV diodes
- Scheduled Work, 1AB EDG, Unit 1 Fall 2014 Refueling Outage  
- WO 55455101, 2-33X-SVC-CL, Remove, Install, and PMT Relay
- Terry Turbine Vendor Manual  
1R20 Outage Activities
- WO 55425039-15, Investigate Governor Valve  
- 12-EHP-4030-002-356, Low Power Physics Tests with Dynamic Rod Worth Measurement,
- WO 55432038-01, Replace 1-CRID-3-INV diodes  
  Revision 11
- WO 55455101, 2-33X-SVC-CL, Remove, Install, and PMT Relay  
- 12-OHP-4021-018-002, Placing In-service the Spent Fuel Pit Cooling and Cleanup System,
1R20 Outage Activities  
  Revision 27
- 12-EHP-4030-002-356, Low Power Physics Tests with Dynamic Rod Worth Measurement,  
- 12-OHP-4050-FHP-023, Reactor Vessel Head Removal with Fuel in the Vessel, Revision 11
Revision 11  
- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11
- 12-OHP-4021-018-002, Placing In-service the Spent Fuel Pit Cooling and Cleanup System,  
- 1-OHP-4021-001-002, Reactor Startup, Revision 52
Revision 27  
- 1-OHP-4021-001-003, Power Reduction, Revision 55
- 12-OHP-4050-FHP-023, Reactor Vessel Head Removal with Fuel in the Vessel, Revision 11  
- 1-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 72
- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11  
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25
- 1-OHP-4021-001-002, Reactor Startup, Revision 52  
- 1-OHP-4021-017-002, Placing Inservice the RHR System, Revision 28
- 1-OHP-4021-001-003, Power Reduction, Revision 55  
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24
- 1-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 72  
- 1-OHP-4030-127-037, Refueling Surveillance, Revision 20
- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25  
- 1-OHP-4030-127-041, Refueling Integrity, Revision 25
- 1-OHP-4021-017-002, Placing Inservice the RHR System, Revision 28  
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35
- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24  
- 1-OHP-5030-001-002, Outage Risk and Technical Specification Monitoring, Revision 20
- 1-OHP-4030-127-037, Refueling Surveillance, Revision 20  
                                              8
- 1-OHP-4030-127-041, Refueling Integrity, Revision 25  
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35  
- 1-OHP-5030-001-002, Outage Risk and Technical Specification Monitoring, Revision 20  


- 2-OHP-4021-001-002, Reactor Startup, Revision 51
- 2-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 60
9
- 2-OHP-4021-017-002, Placing Inservice the RHR System, Revision 24
- AR-2014-12738, 1-NLI-132 Reading Erroneously High, October 16, 2014
- 2-OHP-4021-001-002, Reactor Startup, Revision 51  
- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,
- 2-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 60  
  October 23, 2014
- 2-OHP-4021-017-002, Placing Inservice the RHR System, Revision 24  
- DIT-B-03590-00, Hot Leg Vent Size Required to Prevent RCS Pressurization During Loss of
- AR-2014-12738, 1-NLI-132 Reading Erroneously High, October 16, 2014  
  Shutdown Cooling
- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,  
- Drawing OP-1-12003-33, 250VDC One Line Diagram, Engineered Safety System
October 23, 2014  
- Forced Outage Schedule, November 4, 2014
- DIT-B-03590-00, Hot Leg Vent Size Required to Prevent RCS Pressurization During Loss of  
- PMP-2060-WHL-001, Work Hour Limitation and Fatigue Management, Revision 4
Shutdown Cooling  
- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4
- Drawing OP-1-12003-33, 250VDC One Line Diagram, Engineered Safety System  
- SRP 15.7.4, Radiological Consequences of Fuel Handling Accidents, NUREG-0800
- Forced Outage Schedule, November 4, 2014  
- Tagout R-4KVAC-XFM1-0184, Clearing of Unit 1 and 2 Reserve Feed
- PMP-2060-WHL-001, Work Hour Limitation and Fatigue Management, Revision 4  
- Tagout R-CRID-CRD4-0069, 120VAC Control Room
- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4  
- UFSAR Section 14.2.1.6, Radiological Consequence Analysis, Revision 25
- SRP 15.7.4, Radiological Consequences of Fuel Handling Accidents, NUREG-0800  
- Unit 1 Post Trip Review Report, November 1, 2014 Trip
- Tagout R-4KVAC-XFM1-0184, Clearing of Unit 1 and 2 Reserve Feed  
- Various Working Hour Records, Mechanical Maintenance, Operations, and Electrical
- Tagout R-CRID-CRD4-0069, 120VAC Control Room  
  Maintenance Departments
- UFSAR Section 14.2.1.6, Radiological Consequence Analysis, Revision 25  
1R22 Surveillance Testing
- Unit 1 Post Trip Review Report, November 1, 2014 Trip  
- 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance, Revision 8
- Various Working Hour Records, Mechanical Maintenance, Operations, and Electrical  
- 1-EHP-4030-128-229, Unit 1 Control Room Emergency Ventilation Surveillance,
Maintenance Departments  
  Revision 17-18
1R22 Surveillance Testing  
- 1-EHP-4030-134-203, Unit 1 LLRT, Revision 16
- 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance, Revision 8  
- 1-OHP-4030-108-008R, ECCS Check Valve Test, Revision 19
- 1-EHP-4030-128-229, Unit 1 Control Room Emergency Ventilation Surveillance,  
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35
Revision 17-18  
- 50.59 Screen 2014-0469-00 for Revision 18 to 1-EHP-4030-128-229, Unit 1 Control Room
- 1-EHP-4030-134-203, Unit 1 LLRT, Revision 16  
  Emergency Ventilation Surveillance
- 1-OHP-4030-108-008R, ECCS Check Valve Test, Revision 19
- AR 2014-12787, U1 Ice Condenser Intermediate Deck Doors Exceed Opening Force
- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35  
- AR-2014-11475, 1-IMO-221 Start to Open Time >2 sec
- 50.59 Screen 2014-0469-00 for Revision 18 to 1-EHP-4030-128-229, Unit 1 Control Room  
- AR-2014-11476, 1-FRV-240 Stroked too Slow for ESF test
Emergency Ventilation Surveillance  
- AR-2014-12067, Control Room Emergency Vent Outside Makeup Air Flows Low
- AR 2014-12787, U1 Ice Condenser Intermediate Deck Doors Exceed Opening Force  
- AR-2014-12633, N SI Pump Calculated dP high
- AR-2014-11475, 1-IMO-221 Start to Open Time >2 sec  
- AR-2014-12652, South SI Pump dP High Above Action Limit
- AR-2014-11476, 1-FRV-240 Stroked too Slow for ESF test  
- DIT-S-06286-00, Acceptance of Normal Make Up Air Flow for Unit 1 and Unit 2 Control Room
- AR-2014-12067, Control Room Emergency Vent Outside Makeup Air Flows Low  
  Air Conditioning System
- AR-2014-12633, N SI Pump Calculated dP high  
- Drawing OP-1-5149-48, Control Room Ventilation Unit 1
- AR-2014-12652, South SI Pump dP High Above Action Limit  
- PMP-4030-TRT-001, Time Response and Verification of Engineered Safety Features,
- DIT-S-06286-00, Acceptance of Normal Make Up Air Flow for Unit 1 and Unit 2 Control Room  
  Revision 15
Air Conditioning System  
- Pump and Valve Inservice Test Program for D.C. Cook Nuclear Plant, Fourth Ten Year
- Drawing OP-1-5149-48, Control Room Ventilation Unit 1  
  Interval, Revision 1
- PMP-4030-TRT-001, Time Response and Verification of Engineered Safety Features,  
- WO 55428831, Ice Condenser Intermediate Deck Door Surveillance, October 16, 2014
Revision 15  
- WO 55442013-02, Perform MOV Preventive Maintenance, October 7, 2014
- Pump and Valve Inservice Test Program for D.C. Cook Nuclear Plant, Fourth Ten Year  
- WO 55453695, Ice Condenser Intermediate Deck Door Surveillance, October 18, 2014
Interval, Revision 1  
1EP4 Emergency Action Level and Emergency Plan Changes
- WO 55428831, Ice Condenser Intermediate Deck Door Surveillance, October 16, 2014  
- AR 2014-10545, RP to Evaluate Adequacy of ERO Staffing
- WO 55442013-02, Perform MOV Preventive Maintenance, October 7, 2014  
- AR 2014-15685, Potential EP Finding
- WO 55453695, Ice Condenser Intermediate Deck Door Surveillance, October 18, 2014  
                                              9
1EP4 Emergency Action Level and Emergency Plan Changes  
- AR 2014-10545, RP to Evaluate Adequacy of ERO Staffing  
- AR 2014-15685, Potential EP Finding  


- Emergency Plan, Revision 18, 19, 32, 33, 34, and 35
- PMI-2080, Emergency Plan and Implementing Procedures, Revision 18
10
- Safety Evaluation of Indiana Michigan Power Company Proposed Emergency Plan Changes,
  March 5, 2003
- Emergency Plan, Revision 18, 19, 32, 33, 34, and 35  
2RS1 Radiological Hazard Assessment and Exposure Controls
- PMI-2080, Emergency Plan and Implementing Procedures, Revision 18  
- 12-THP-6010- RPP-104, Personnel Dosimetry Use in Varying Radiation, Revision 15
- Safety Evaluation of Indiana Michigan Power Company Proposed Emergency Plan Changes,  
- 12-THP-6010- RPP-407, Special Radiological Evolutions, Revision 28
March 5, 2003  
- 12-THP-6010-RPP-006, Radiation Work Permit Processing, Revision 34
2RS1 Radiological Hazard Assessment and Exposure Controls  
- 12-THP-6010-RPP-314, Pressure Washing of Plant Components and Structures, Revision 8
- 12-THP-6010- RPP-104, Personnel Dosimetry Use in Varying Radiation, Revision 15  
- 12-THP-6010-RPP-401, Performance of Radiation and Contamination Surveys, Revision 36
- 12-THP-6010- RPP-407, Special Radiological Evolutions, Revision 28  
- 12-THP-6010-RPP-405, Analysis of Airborne Radioactivity, Revision 19
- 12-THP-6010-RPP-006, Radiation Work Permit Processing, Revision 34  
- 12-THP-6010-RPP-420, Radiological Controls for Radiography, Revision 6
- 12-THP-6010-RPP-314, Pressure Washing of Plant Components and Structures, Revision 8  
- 12-THP-6010-RPP-421, Radiological Controls for Steam Generator Maintenance, Revision 7
- 12-THP-6010-RPP-401, Performance of Radiation and Contamination Surveys, Revision 36  
- 55399455-88, Radiography Shot Plan of Unit 1 West Containment Spray Heat Exchanger
- 12-THP-6010-RPP-405, Analysis of Airborne Radioactivity, Revision 19  
  Room and Shot Plan of Elevation 609 E/W Hallway, October 10, 2014
- 12-THP-6010-RPP-420, Radiological Controls for Radiography, Revision 6  
- AR 2013-13969, Electronic Dosimeter Setpoints Often Set Considerably Higher Than Actual or
- 12-THP-6010-RPP-421, Radiological Controls for Steam Generator Maintenance, Revision 7  
  Expected Radiological Conditions
- 55399455-88, Radiography Shot Plan of Unit 1 West Containment Spray Heat Exchanger  
- AR 2013-5450, Dose and Dose Rate Alarm Setpoints are Potentially too High
Room and Shot Plan of Elevation 609 E/W Hallway, October 10, 2014  
- AR 2014-11295, An Untrained Worker Entered the Restricted Area on the Wrong RWP
- AR 2013-13969, Electronic Dosimeter Setpoints Often Set Considerably Higher Than Actual or  
- AR 2014-11975, Dose Alarm
Expected Radiological Conditions  
- AR 2014-8964, Rad Worker Deficiency
- AR 2013-5450, Dose and Dose Rate Alarm Setpoints are Potentially too High  
- AR 2014-9001, New Supplemental Locked High Radiation Area Ladder Cover Not Engrained
- AR 2014-11295, An Untrained Worker Entered the Restricted Area on the Wrong RWP  
  in Process
- AR 2014-11975, Dose Alarm  
- AR 2014-9764, A Review of ED Setpoints
- AR 2014-8964, Rad Worker Deficiency  
- CNP-1311-0001 Survey Unit 2 Upper Cavity, November 1, 2013
- AR 2014-9001, New Supplemental Locked High Radiation Area Ladder Cover Not Engrained  
- CNP-1311-0012 Survey Unit 2 Upper Cavity, October 31, 2013
in Process  
- PMP-6010-RPP-003, Data Sheet 4, Down Posting the Reactor Pit Area, October 16, 2014
- AR 2014-9764, A Review of ED Setpoints  
- PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, Revision 23
- CNP-1311-0001 Survey Unit 2 Upper Cavity, November 1, 2013  
- PMP-6010-RPP-006, Data Sheet 2, Pre-Job ALARA Briefing Checklist, Down Post Survey of
- CNP-1311-0012 Survey Unit 2 Upper Cavity, October 31, 2013  
  the Rx Pit, October 16, 2014
- PMP-6010-RPP-003, Data Sheet 4, Down Posting the Reactor Pit Area, October 16, 2014  
- PMP-6010-RPP-006, Radiation Work Permit Program, Revision 19
- PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, Revision 23  
- RWP 1 41130, U1C26 - Perform Radiography in Auxiliary & Turbine Buildings & Plant
- PMP-6010-RPP-006, Data Sheet 2, Pre-Job ALARA Briefing Checklist, Down Post Survey of  
  Restricted Areas, Revision 0
the Rx Pit, October 16, 2014  
- RWP 141100, U1C26 - Refuel Cavity Decontamination Activities, Revision 0
- PMP-6010-RPP-006, Radiation Work Permit Program, Revision 19  
- RWP 141121, U1C26 - Auxiliary Building & Restricted Area Minor Engineering Change
- RWP 1 41130, U1C26 - Perform Radiography in Auxiliary & Turbine Buildings & Plant  
  Modifications and Support Work, Revision 0
Restricted Areas, Revision 0  
- RWP 141123, Install, Remove, Modify Temporary Shielding in Unit-1 Containment, Auxiliary
- RWP 141100, U1C26 - Refuel Cavity Decontamination Activities, Revision 0  
  Building and Plant Restricted Areas, and ALARA Plan, Revision 0
- RWP 141121, U1C26 - Auxiliary Building & Restricted Area Minor Engineering Change  
- RWP 141145, U1C26 - Valve Maintenance / Repair, Revision 2
Modifications and Support Work, Revision 0  
- RWP 141148, U1C26 - Steam Generator Platform Activities, Revision 2
- RWP 141123, Install, Remove, Modify Temporary Shielding in Unit-1 Containment, Auxiliary  
- RWP 141172, U1C26 - Reactor Pit VHRA Down-post Survey, Revision 0
Building and Plant Restricted Areas, and ALARA Plan, Revision 0  
- RWP 141187, U1C26 - Under Rx Vessel Inspections, Revision 0
- RWP 141145, U1C26 - Valve Maintenance / Repair, Revision 2  
- Survey SW VSDS-M-20144116-9, Critical Survey - Down Posting the Reactor Pit,
- RWP 141148, U1C26 - Steam Generator Platform Activities, Revision 2  
  October 16, 2014
- RWP 141172, U1C26 - Reactor Pit VHRA Down-post Survey, Revision 0  
- SW_VSDS-M-20140923-1, Unit 1 Containment Spray Heat Exchanger Rooms Survey
- RWP 141187, U1C26 - Under Rx Vessel Inspections, Revision 0  
- THG-026, Locked High Radiation Area and Very-High Radiation Weekly Verification Process,
- Survey SW VSDS-M-20144116-9, Critical Survey - Down Posting the Reactor Pit,
  Revision 14
October 16, 2014  
- Work Order Package 55446099 01, RP Perform Semiannual Source Inventory,
- SW_VSDS-M-20140923-1, Unit 1 Containment Spray Heat Exchanger Rooms Survey  
  August 7, 2014
- THG-026, Locked High Radiation Area and Very-High Radiation Weekly Verification Process,  
                                              10
Revision 14  
- Work Order Package 55446099 01, RP Perform Semiannual Source Inventory,  
August 7, 2014  


2RS2 Occupational ALARA Planning and Controls
- ALARA Committee Meeting; A-14-33F; October 15, 2014
11
- D.C. Cook U1R26; ALARA Review Committee; RWP 141148 & 141149; October 15, 2014
- Full Self-Assessment Report; ALARA Program Implementation; 2014-0265; September 29, 2014
2RS2 Occupational ALARA Planning and Controls  
- PMP-6010-ALA-001; ALARA Program - Review of Plant Work Activities; Revision 27
- ALARA Committee Meeting; A-14-33F; October 15, 2014  
2RS7 Radiological Environmental Monitoring Program
- D.C. Cook U1R26; ALARA Review Committee; RWP 141148 & 141149; October 15, 2014  
- 12 THP-6010 RPC-538, Calibration of the F&J DF-1 Low Volume Air Sampler, Revision 2
- Full Self-Assessment Report; ALARA Program Implementation; 2014-0265; September 29, 2014  
- 12 THP-6010-RPP-630, Collection of Surface Water Samples, 007
- PMP-6010-ALA-001; ALARA Program - Review of Plant Work Activities; Revision 27  
- 12 THP-6010-RPP-632, Collection of Environmental Air Samples, Revision 010
2RS7 Radiological Environmental Monitoring Program  
- 12 THP-6010-RPP-638, Collection of Grape and Broadleaf Samples, Revision 007
- 12 THP-6010 RPC-538, Calibration of the F&J DF-1 Low Volume Air Sampler, Revision 2  
- 12 THP-6010-RPP-642, Collection of Drinking Water Samples, Revision 007
- 12 THP-6010-RPP-630, Collection of Surface Water Samples, 007  
- 12-IHP-4030-036-001, Meteorological Instrumentation - Primary And Backup Towers Channel
- 12 THP-6010-RPP-632, Collection of Environmental Air Samples, Revision 010  
  Calibration, Revision 0
- 12 THP-6010-RPP-638, Collection of Grape and Broadleaf Samples, Revision 007  
- 12-IHP-6030-036-00, Shoreline Weather Tower Instrument Calibration, Revision 000
- 12 THP-6010-RPP-642, Collection of Drinking Water Samples, Revision 007  
- 12-THP-6020-INS-525, Liquid Scintillation Counter, Revision 009
- 12-IHP-4030-036-001, Meteorological Instrumentation - Primary And Backup Towers Channel  
- 12-THP-6020-INS-526, Gamma Spectrometry Using Ortec Global Value and Gamma Vision
Calibration, Revision 0  
  Software, Revision 002
- 12-IHP-6030-036-00, Shoreline Weather Tower Instrument Calibration, Revision 000  
- 2013 Radiological Environmental Monitoring Program Land Use Census, September 24, 2013
- 12-THP-6020-INS-525, Liquid Scintillation Counter, Revision 009  
- Annual Radiological Environmental Operating Report, Donald C. Cook Nuclear Plant
- 12-THP-6020-INS-526, Gamma Spectrometry Using Ortec Global Value and Gamma Vision  
  Radiological Environmental Monitoring Program, January 1, 2013 - December 31, 2013
Software, Revision 002  
- AR 2013-10179, ONS-5 Air Station Was Out of Service for Approximately 37.5 Hours
- 2013 Radiological Environmental Monitoring Program Land Use Census, September 24, 2013  
- AR 2013-15116, MET Tower Data Recovery
- Annual Radiological Environmental Operating Report, Donald C. Cook Nuclear Plant  
- AR 2013-3738, Quarterly Radiological Environmental Monitoring Program (REMP) TLD
Radiological Environmental Monitoring Program, January 1, 2013 - December 31, 2013  
  Collection and Change Out, TLD T-11 Could Not Be Located
- AR 2013-10179, ONS-5 Air Station Was Out of Service for Approximately 37.5 Hours  
- AR 2013-6824, ONS-1 Air Station was Out of Service for Approximately 2.5 Hours
- AR 2013-15116, MET Tower Data Recovery  
- AR 2013-7934, COL (Coloma) Air Station was Out of Service For Approximately 0.5 Hours
- AR 2013-3738, Quarterly Radiological Environmental Monitoring Program (REMP) TLD  
- AR 2014-10063, 12-ELR-400, East Bucket Heater Broken
Collection and Change Out, TLD T-11 Could Not Be Located  
- AR 2014-11607, Environmental Technician was Notified That the Control Farm Would No
- AR 2013-6824, ONS-1 Air Station was Out of Service for Approximately 2.5 Hours  
  Longer Produce Milk
- AR 2013-7934, COL (Coloma) Air Station was Out of Service For Approximately 0.5 Hours  
- AR 2014-13656, Trace Cesium-137 in Broadleaf Sample
- AR 2014-10063, 12-ELR-400, East Bucket Heater Broken  
- AR 2014-5725, First Quarter of 2014, With The Exception Of Two Days (March 23 And 24),
- AR 2014-11607, Environmental Technician was Notified That the Control Farm Would No  
  Ice Build Up On Lake Michigan Prevented the Collection of Radiological Environmental
Longer Produce Milk  
  Monitoring Program (REMP) Surface Water Samples,
- AR 2014-13656, Trace Cesium-137 in Broadleaf Sample  
- AR 2014-6725 Radiological Environmental Monitoring Program (REMP) Air Station ONS-1
- AR 2014-5725, First Quarter of 2014, With The Exception Of Two Days (March 23 And 24),  
  Lost Power for Approximately 39 minutes
Ice Build Up On Lake Michigan Prevented the Collection of Radiological Environmental  
- AR 2014-8378, Document Results Of The Weekly Review Of Radiological Environmental
Monitoring Program (REMP) Surface Water Samples,  
  Monitoring Program (REMP) Data
- AR 2014-6725 Radiological Environmental Monitoring Program (REMP) Air Station ONS-1  
- AR 2014-8622, Primary Met Tower Carriage Control Switch
Lost Power for Approximately 39 minutes  
- AR2013-12672, Evaluate Siting of ONS-2 and ONS-6
- AR 2014-8378, Document Results Of The Weekly Review Of Radiological Environmental  
- D. C. Cook Nuclear Plant Updated Final Safety Analysis Report, Section 11.0, Waste Disposal
Monitoring Program (REMP) Data  
  and Radiation Protection System, Revision 25.0
- AR 2014-8622, Primary Met Tower Carriage Control Switch  
- PA-13-01, Performance Assurance Audit, Radiological Environmental Monitoring Program and
- AR2013-12672, Evaluate Siting of ONS-2 and ONS-6  
  Offsite Dose Calculation Manual, March 1, 2013
- D. C. Cook Nuclear Plant Updated Final Safety Analysis Report, Section 11.0, Waste Disposal  
- PMP-6010-OSD-001, Off-Site Dose Calculation Manual, Revision 24
and Radiation Protection System, Revision 25.0  
- WO 554444469, Meteorological Instrumentation Calibration, October 11, 2014
- PA-13-01, Performance Assurance Audit, Radiological Environmental Monitoring Program and  
                                              11
Offsite Dose Calculation Manual, March 1, 2013  
- PMP-6010-OSD-001, Off-Site Dose Calculation Manual, Revision 24  
- WO 554444469, Meteorological Instrumentation Calibration, October 11, 2014  


4OA1 Performance Indicator Verification
- Dose Calculations and Dose Projections Due to Liquid and Gaseous Effluents for D.C. Cook
12
  Plant, July, 2013 to September 14, 2014
- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly
4OA1 Performance Indicator Verification  
  Operation Report Data, Reactor Coolant System Specific Activity, Revision 15
- Dose Calculations and Dose Projections Due to Liquid and Gaseous Effluents for D.C. Cook  
- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly
Plant, July, 2013 to September 14, 2014  
  Operating Report Data, Revision 15
- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly  
4OA2 Identification and Resolution of Problems
Operation Report Data, Reactor Coolant System Specific Activity, Revision 15  
- 12-OHP-4025-001-002, Fire Response Guidelines, Revision 6
- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly  
- AR 2014-11148, Worker Bumped Detector 3-12 Sends Fire Alarm to U-1 Control Room
Operating Report Data, Revision 15  
- AR 2014-9531, 1-152-CICE4-2A Out of Position
4OA2 Identification and Resolution of Problems  
- AR-2012-8187, Adequacy of Past Operability Questioned
- 12-OHP-4025-001-002, Fire Response Guidelines, Revision 6  
- AR-2013-8600, Fire Zone 79 EDG Corridor Fire with Simultaneous CO2 Actuation
- AR 2014-11148, Worker Bumped Detector 3-12 Sends Fire Alarm to U-1 Control Room
- AR-2013-9251, Inadequate Calculations for ICP-0083 Revision 0 12-ZPS-411
- AR 2014-9531, 1-152-CICE4-2A Out of Position  
- AR-2014-10600, Difference Between Fire Pump Performance in Hydraulic Calcs
- AR-2012-8187, Adequacy of Past Operability Questioned  
- AR-2014-14920, Racking Interlocks Potential to not Properly Reset
- AR-2013-8600, Fire Zone 79 EDG Corridor Fire with Simultaneous CO2 Actuation  
- AR-2014-14951, Primary Coolant Filters Wrong Parts
- AR-2013-9251, Inadequate Calculations for ICP-0083 Revision 0 12-ZPS-411  
- AR-2014-15040, Missing Sheet Metal Screws on Room Cooler Housing
- AR-2014-10600, Difference Between Fire Pump Performance in Hydraulic Calcs  
- AR-2014-15059, Cable 2-8167G Low Megger Readings
- AR-2014-14920, Racking Interlocks Potential to not Properly Reset  
- AR-2014-15087, Fire Pump Setpoint and New TRM Sprinkler Demand
- AR-2014-14951, Primary Coolant Filters Wrong Parts  
- GT-2014-11170-3, Work Order Task Package Quality QHSA Report, October 30, 2014
- AR-2014-15040, Missing Sheet Metal Screws on Room Cooler Housing  
- Performance Assurance Audit PA-14-07, Operations, August 25, 2014
- AR-2014-15059, Cable 2-8167G Low Megger Readings  
- Performance Assurance Quarterly Report, April - June 2014
- AR-2014-15087, Fire Pump Setpoint and New TRM Sprinkler Demand  
- Performance Assurance Quarterly Report, July - September 2014
- GT-2014-11170-3, Work Order Task Package Quality QHSA Report, October 30, 2014  
- Performance Assurance Surveillance, PA-SA-14-001, U1C26 Refueling Outage,
- Performance Assurance Audit PA-14-07, Operations, August 25, 2014  
  November 3, 2014
- Performance Assurance Quarterly Report, April - June 2014  
- Unit 1 and Unit 2 Contingency/Compensatory Actions, December 4, 2014
- Performance Assurance Quarterly Report, July - September 2014  
- Unit 1 and Unit 2 Operator Burden Report, November 18, 2014 and December 4, 2014
- Performance Assurance Surveillance, PA-SA-14-001, U1C26 Refueling Outage,  
- Unit 1 and Unit 2 Supervisor Turnover Checklist, December 4, 2014
November 3, 2014  
4OA3 Identification and Resolution of Problems
- Unit 1 and Unit 2 Contingency/Compensatory Actions, December 4, 2014  
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7
- Unit 1 and Unit 2 Operator Burden Report, November 18, 2014 and December 4, 2014  
- AR 2014-13669 Task 2, Unit 1 Post-trip Report
- Unit 1 and Unit 2 Supervisor Turnover Checklist, December 4, 2014  
- AR 2014-13669 Task 3, Unit 2 Post-trip Report
4OA3 Identification and Resolution of Problems  
- E-0, Reactor Trip or Safety Injection, Revision 38
- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7  
- ES-0.1, Reactor Trip Response, Revision 28
- AR 2014-13669 Task 2, Unit 1 Post-trip Report  
- Ltr Lee Baun to Cook Leadership, Performance Assurance Semi-Monthly Roll-Up Report,
- AR 2014-13669 Task 3, Unit 2 Post-trip Report  
  December 22, 2014
- E-0, Reactor Trip or Safety Injection, Revision 38  
                                                12
- ES-0.1, Reactor Trip Response, Revision 28  
- Ltr Lee Baun to Cook Leadership, Performance Assurance Semi-Monthly Roll-Up Report,  
December 22, 2014


                          LIST OF ACRONYMS USED
ADAMS Agencywide Document Access Management System
13
AFW   Auxiliary Feedwater
ALARA As-Low-As-Reasonably-Achievable
LIST OF ACRONYMS USED  
AMB   Auxiliary Missile Blocks
ADAMS  
AR     Action Request
Agencywide Document Access Management System  
ASME   American Society for Mechanical Engineers
AFW  
BACC   Boric Acid Corrosion Control
Auxiliary Feedwater  
CAP   Corrective Action Program
ALARA  
CAQ   Condition Adverse to Quality
As-Low-As-Reasonably-Achievable  
CDF   Core Damage Frequency
AMB  
CFR   Code of Federal Regulations
Auxiliary Missile Blocks  
dpm   drops per minute
AR  
EAC   Environmental Assessment Coordinator
Action Request  
EDG   Emergency Diesel Generator
ASME
EPRI   Electric Power Research Institute
American Society for Mechanical Engineers  
ET     Eddy Current
BACC  
FME   Foreign Material Exclusion
Boric Acid Corrosion Control  
FOST   Fuel Oil Storage Tank
CAP  
ISI   Inservice Inspection
Corrective Action Program  
LBLOCA Large Break Loss-of-Coolant Accident
CAQ  
LHRA   Locked High Radiation Area
Condition Adverse to Quality  
LOCA   Loss-of-Coolant Accident
CDF  
IMC   Inspection Manual Chapter
Core Damage Frequency  
IP     Inspection Procedure
CFR  
IR     Inspection Report
Code of Federal Regulations  
LCO   Limiting Condition for Operation
dpm  
MDAFW Motor-Driven Auxiliary Feedwater
drops per minute  
MSPI   Mitigating Systems Performance Index
EAC  
NCV   Non- Violation
Environmental Assessment Coordinator  
NDE   Non-destructive Examination
EDG  
NEI   Nuclear Energy Institute
Emergency Diesel Generator  
NRC   U.S. Nuclear Regulatory Commission
EPRI  
PARS   Publicly Available Records System
Electric Power Research Institute  
PI     Performance Indicator
ET  
RAC   Radiological Assessment Coordinator
Eddy Current
RCS   Reactor Coolant System
FME  
RG     Regulatory Guide
Foreign Material Exclusion  
RPT   Radiation Protection Technician
FOST  
SDP   Significance Determination Process
Fuel Oil Storage Tank  
SG     Steam Generator
ISI  
SRA   Senior Reactor Analyst
Inservice Inspection  
SSC   Structure, System and Component
LBLOCA  
TDAFW Turbine-Driven Auxiliary Feedwater
Large Break Loss-of-Coolant Accident  
TS     Technical Specification
LHRA  
                                        13
Locked High Radiation Area  
LOCA  
Loss-of-Coolant Accident  
IMC  
Inspection Manual Chapter  
IP  
Inspection Procedure  
IR  
Inspection Report  
LCO  
Limiting Condition for Operation  
MDAFW  
Motor-Driven Auxiliary Feedwater  
MSPI  
Mitigating Systems Performance Index  
NCV  
Non- Violation  
NDE  
Non-destructive Examination  
NEI  
Nuclear Energy Institute  
NRC  
U.S. Nuclear Regulatory Commission  
PARS  
Publicly Available Records System  
PI  
Performance Indicator  
RAC  
Radiological Assessment Coordinator  
RCS  
Reactor Coolant System  
RG  
Regulatory Guide  
RPT  
Radiation Protection Technician  
SDP  
Significance Determination Process  
SG  
Steam Generator  
SRA  
Senior Reactor Analyst  
SSC  
Structure, System and Component  
TDAFW  
Turbine-Driven Auxiliary Feedwater  
TS  
Technical Specification


TTV   Trip and Throttle Valve
UFSAR Updated Final Safety Analysis Report
14
URI   Unresolved Item
UT   Ultrasonic Test
TTV  
WO   Work Order
Trip and Throttle Valve  
                                    14
UFSAR  
Updated Final Safety Analysis Report  
URI  
Unresolved Item  
UT  
Ultrasonic Test  
WO  
Work Order  


L. Weber                                                                   -2-
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy
L. Weber  
of this letter, its enclosure, and your response (if any) will be available electronically for public
-2-  
inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)
component of the NRC's Agencywide Documents Access and Management System (ADAMS).
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public  
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy  
(the Public Electronic Reading Room).
of this letter, its enclosure, and your response (if any) will be available electronically for public  
                                                                          Sincerely,
inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)  
                                                                          /RA/
component of the NRC's Agencywide Documents Access and Management System (ADAMS).
                                                                          Kenneth Riemer, Chief
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html  
                                                                          Branch 2
(the Public Electronic Reading Room).  
                                                                          Division of Reactor Projects
Sincerely,  
Docket Nos. 50-315; 50-316
License Nos. DPR-58; DPR-74
/RA/  
Enclosure:
IR 05000315/2014005; 05000316/2014005
    w/Attachment: Supplemental Information
Kenneth Riemer, Chief  
cc w/encl: Distribution via LISTSERV
Branch 2  
DISTRIBUTION w/encl:
Division of Reactor Projects  
Kimyata MorganButler                                                                   Carole Ariano
RidsNrrDorlLpl3-1 Resource                                                             Linda Linn
Docket Nos. 50-315; 50-316  
RidsNrrPMDCCook Resource                                                               DRPIII
License Nos. DPR-58; DPR-74  
RidsNrrDirsIrib Resource                                                               DRSIII
Cynthia Pederson                                                                       Jim Clay
Enclosure:  
Darrell Roberts                                                                        Carmen Olteanu
Eric Duncan                                                                            ROPreports.Resource@nrc.gov
IR 05000315/2014005; 05000316/2014005  
Allan Barker
w/Attachment: Supplemental Information  
ADAMS Accession Number:
cc w/encl: Distribution via LISTSERV  
    Publicly Available                           Non-Publicly Available                             Sensitive                       Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
DISTRIBUTION w/encl:  
  OFFICE             RIII                               RIII-EICS                       RIII                               RIII
Kimyata MorganButler  
  NAME               NS:rj                               PLougheed for                   KRiemer
RidsNrrDorlLpl3-1 Resource
                                                        EDuncan
RidsNrrPMDCCook Resource  
  DATE               02/09/15                           02/09/15                         02/10/15
RidsNrrDirsIrib Resource  
                                                          OFFICIAL RECORD COPY
Cynthia Pederson  
Darrell Roberts
Eric Duncan
Allan Barker
Carole Ariano
Linda Linn
DRPIII
DRSIII
Jim Clay  
Carmen Olteanu  
ROPreports.Resource@nrc.gov  
ADAMS Accession Number:  
Publicly Available  
Non-Publicly Available  
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Non-Sensitive  
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy  
   
OFFICE  
RIII  
RIII-EICS  
RIII  
RIII  
   
NAME  
NS:rj  
PLougheed for  
EDuncan
KRiemer  
   
DATE  
02/09/15  
02/09/15  
02/10/15  
OFFICIAL RECORD COPY
}}
}}

Latest revision as of 14:26, 10 January 2025

IR 05000315/2014005, 05000316/2014005; on 10/01/2014 - 12/31/2014; Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional Assessments; Plant Modifications; Post Maintenance Testing; Radiological Hazard
ML15042A380
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 02/10/2015
From: Kenneth Riemer
NRC/RGN-III/DRP/B2
To: Weber L
Indiana Michigan Power Co, Nuclear Generation Group
References
IR 2014005
Download: ML15042A380 (69)


See also: IR 05000315/2014005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE RD. SUITE 210

LISLE, IL 60532-4352

February 10, 2015

Mr. Larry Weber

Senior VP and Chief Nuclear Officer

Indiana Michigan Power Company

Nuclear Generation Group

One Cook Place

Bridgman, MI 49106

SUBJECT: DONALD C. COOK NUCLEAR POWER PLANT, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000315/2014005;

05000316/2014005

Dear Mr. Weber:

On December 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Donald C. Cook Nuclear Power Plant, Units 1 and 2. The enclosed report

documents the results of this inspection, which were discussed on January 20, 2015, with

yourself and members of your staff.

Based on the results of this inspection, three NRC-identified and two self-revealed findings of

very low safety significance were identified. The findings involved violations of NRC

requirements. However, because of their very low safety significance, and because the issues

were entered into your corrective action program, the NRC is treating the issues as

non-cited violations (NCVs) in accordance with Section 2.3.2 of the NRC Enforcement Policy

If you contest the subject or severity of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Donald C. Cook Nuclear Power Plant. In addition, if you disagree with the

cross-cutting aspect assigned to any finding in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement, to the

Regional Administrator, Region III, and the NRC Resident Inspector at the Donald C. Cook

Nuclear Power Plant.

L. Weber

-2-

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy

of this letter, its enclosure, and your response (if any) will be available electronically for public

inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)

component of the NRC's Agencywide Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket Nos. 50-315; 50-316

License Nos. DPR-58; DPR-74

Enclosure:

IR 05000315/2014005; 05000316/2014005

w/Attachment: Supplemental Information

cc w/encl: Distribution via LISTSERV

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

05000315; 05000316

License Nos:

DPR-58; DPR-74

Report No:

05000315/2014005; 05000316/2014005

Licensee:

Indiana Michigan Power Company

Facility:

Donald C. Cook Nuclear Power Plant, Units 1 and 2

Location:

Bridgman, MI

Dates:

October 1 through December 31, 2014

Inspectors:

J. Ellegood, Senior Resident Inspector

T. Taylor, Resident Inspector

J. Cassidy, Senior Health Physicist

M. Garza, Emergency Response Specialist

T. Go, Health Physicist

J. Lennartz, Project Engineer

M. Mitchell, Health Physicist

M. Phalen, Senior Health Physicist

E. Sanchez Santiago, Reactor Inspector

Approved by:

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 2

REPORT DETAILS ....................................................................................................................... 6

Summary of Plant Status ........................................................................................................... 6

1.

REACTOR SAFETY ................................................................................................. 6

1R01

Adverse Weather Protection (71111.01) ............................................................ 6

1R04

Equipment Alignment (71111.04) ....................................................................... 7

1R05

Fire Protection (71111.05) .................................................................................. 8

1R06

Flooding (71111.06) ........................................................................................... 9

1R07

Annual Heat Sink Performance (71111.07) ...................................................... 10

1R08

Inservice Inspection Activities (71111.08P) ...................................................... 10

1R11

Licensed Operator Requalification Program (71111.11) .................................. 13

1R12

Maintenance Effectiveness (71111.12) ............................................................ 15

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13) ....... 15

1R15

Operability Determinations and Functional Assessments (71111.15) .............. 16

1R18

Plant Modifications (71111.18) ......................................................................... 21

1R19

Post-Maintenance Testing (71111.19) ............................................................. 24

1R20

Outage Activities (71111.20) ............................................................................ 27

1R22

Surveillance Testing (71111.22) ....................................................................... 28

1EP4

Emergency Action Level and Emergency Plan Changes (71114.04) ............... 29

2.

RADIATION SAFETY ............................................................................................. 31

2RS1

Radiological Hazard Assessment and Exposure Controls (71124.01) ............. 31

2RS2

Occupational As-Low-As-Reasonably-Achievable Planning and Controls

(71124.02) ........................................................................................................ 37

2RS7

Radiological Environmental Monitoring Program (71124.07) ........................... 38

4.

OTHER ACTIVITIES .............................................................................................. 40

4OA1

Performance Indicator Verification (71151) ...................................................... 40

4OA2

Identification and Resolution of Problems (71152) ........................................... 45

4OA3

Followup of Events and Notices of Enforcement Discretion (71153) ............... 49

4OA6

Management Meetings ..................................................................................... 50

SUPPLEMENTAL INFORMATION ............................................................................................... 1

KEY POINTS OF CONTACT..................................................................................................... 1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 2

LIST OF DOCUMENTS REVIEWED ......................................................................................... 3

LIST OF ACRONYMS USED .................................................................................................. 13

2

SUMMARY OF FINDINGS

Inspection Report 05000315/2014005, 05000316/2014005; 10/01/2014 - 12/31/2014;

Donald C. Cook Nuclear Power Plant, Units 1 and 2; Operability Determinations and Functional

Assessments; Plant Modifications; Post-Maintenance Testing; Radiological Hazard Assessment

and Exposure Controls.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Three Green findings were identified by the

inspectors. Additionally, there were two Green self-revealed findings. The findings were

considered non-cited violations (NCVs) of NRC regulations. The significance of inspection

findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and

determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Aspects Within the

Cross-Cutting Areas effective date December 4, 2014. All violations of NRC requirements are

dispositioned in accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRC's

program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 5, dated February 2014.

Cornerstone: Mitigating Systems

Green. A finding of very low safety significance, with an associated non-cited violation of

10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the

inspectors for the licensees failure to promptly identify and correct a condition adverse

to quality (CAQ) associated with Unit 1 Turbine-Driven Auxiliary Feedwater (TDAFW)

pump turbine bearing oil. Specifically, the licensee failed to identify that water was

entering the oil system after leakage had been identified directly above one of the

TDAFW pump turbine bearings. On April 7, 2014, a cooling water leak was identified

above the outboard turbine bearing. The leak was classified as about 1 drop-per-minute

(dpm). On April 11, 2014, the licensee discovered the turbine bearing oil level was

above the maximum mark on an attached sight glass. Several possible reasons were

postulated for the high level (which had been steady in-band for over a year), such as

rising turbine building temperatures and the fact that it was not uncommon for personnel

to do unnecessary oil adds to the machine. Oil was drained out until level returned to

the maximum mark. On May 22, 2014, the licensee again noted oil level to be above the

maximum mark. Oil was drained again, and similar reasons provided for the level

increase. Further, a statement was made that oil level had been steady for the past

month, neglecting the previous high level condition. In parallel, NRC inspectors had

questioned why level was being maintained at the maximum mark when the operator

logs and a sign stated level should be kept at the minimum mark. On May 23, the

licensee decided to drain the oil system; 620 ml of water was found. New oil was added,

and a temporary modification was installed which directed leakage away from the

bearing. The issue was entered into the Corrective Action Program (CAP), and an

apparent cause evaluation later determined the leakage to be the primary intrusion

pathway for the water.

The issue was more-than-minor because it adversely affected the Configuration Control

attribute of the Mitigating Systems Cornerstone, whose objective is to ensure the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Additionally, if left uncorrected, the issue could lead

to a more significant safety concern. The inspectors assessed the finding for

3

significance using IMC 0609, Significance Determination Process. Per Appendix A, the

finding screened as Green, or very low safety significance, in Exhibit 2. Specifically, all

questions were answered no under Section A for findings related to Mitigating

Structures, Systems and Components (SSCs) and Functionality. The inspectors

reviewed the licensees past operability evaluation and concluded that given the

projected amount of water that could be entrained in the oil during operation, along with

the duration of operation assumed in the safety analyses, that operability of the pump

would be maintained. The finding had an associated cross-cutting aspect in the Human

Performance area, specifically, H.11, Challenge the Unknown. Regarding the TDAFW

oil system, the licensee rationalized why the level was increasing without sufficient

investigation given the significance of the system, and did not seek further information

that was readily available regarding appropriate oil levels. (Section 1R15)

Green. A finding of very low safety significance, with an associated non-cited violation

of Technical Specification (TS) 5.4, Procedures, was self-revealed when a vacuum was

inadvertently drawn on the AB Fuel Oil Storage Tank (FOST) during preparations for

surveillance activities. The vacuum caused an indication of lowering level in the tank,

alarms, and an unplanned TS Limiting Condition for Operation (LCO) action statement

entry. The licensee was performing work activities in preparation for a leak test of the

FOST. The general sequence of activities should have been a loosening of the vent

filter for the tank, a transfer of fuel from the FOST to the Emergency Diesel Generator

(EDG) day tanks, removal of the FOST from service, and finally removal of the vent filter

so test equipment could be connected to the tank. Due to ambiguous work instruction

steps and activities not being adequately controlled to ensure the proper sequence

occurred, workers first removed the vent filter completely and placed a Foreign Material

Exclusion (FME) bag over the vent. When operators later transferred fuel, a vacuum

was drawn in the tank and level appeared to be going down. Utilizing a manual method

of level measurement (which had also been affected by the vacuum), operators

determined fuel was actually being lost from the tank to the environment. Shortly

thereafter, the bag was found and removed, and level restored to normal (there was no

actual loss of fuel). Technical Specification 5.4, Procedures, states, in part, that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in

part, that maintenance that can affect the performance of safety-related equipment

should be properly preplanned and performed in accordance with written procedures,

documented instructions, or drawings appropriate to the circumstances. Contrary to

these requirements, the FOST surveillance was performed with inadequate instructions

and was not coordinated appropriately. The licensee entered the issue into the CAP and

performed a root cause analysis.

The performance deficiency was more than minor because it adversely impacted the

Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is

ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. The finding screened as Green, or very

low safety significance, utilizing IMC 0609, Appendix A, The Significance Determination

Process for Findings at Power. Specifically, all questions were answered no under

Section A of Exhibit 2 for Mitigating Systems, since that was the affected cornerstone.

The FME bag was installed, which rendered the AB FOST inoperable, for approximately

16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. This was less than the TS allowed outage time of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. The finding had

an associated cross-cutting aspect in the human performance area, specifically, H.5,

Work Management. Work activities should be planned, controlled, and executed with

4

nuclear safety as the overriding priority. Contrary to the tenets of the cross-cutting

aspect, the work was planned and executed with inadequate work instructions. Further,

there was a lack of coordination between a number of work groups and activities

associated with the test. (Section 1R15)

Green. A finding of very low safety significance, with an associated non- violation

of TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1

TDAFW pump tripped during an emergent dual-unit shutdown. Both units were taken

offline by operators due to debris intrusion from Lake Michigan into the cooling water

screenhouse. The TDAFW pump started as expected but shutdown after a few minutes

of operation. Investigation by the licensee revealed that a cover for the trip solenoid had

been installed incorrectly. The cover was relatively loose and had been placed near

components involved with the proper latching of the Trip and Throttle valve (TTV) (the

valve which opens to let steam in to turn the pump on). After refuting several possible

causes and running the pump several times for testing, the licensee determined the

likely cause of the trip was the misplaced enclosure, which could have interfered with the

proper latching of the TTV. Technical Specification 5.4, Procedures, states, in part,

that written procedures shall be established, implemented, and maintained covering the

applicable procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33

states, in part, that maintenance that can affect the performance of safety-related

equipment should be properly preplanned and performed in accordance with written

procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to these requirements, the cause of the misplaced enclosure was due to a lack

of detailed instructions regarding the installation and removal of the enclosure. The

enclosure was most recently affected by maintenance performed during the fall 2014

refueling outage. The licensee worked with the vendor and reinstalled the enclosure

correctly. The Unit 2 TDAFW pump trip solenoid enclosure was also found out of

position and corrected. The licensee entered the issue into the CAP.

The performance deficiency was more than minor because it adversely impacted the

Configuration Control attribute of the Mitigating Systems cornerstone, whose objective is

ensuring the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. The inspectors utilized IMC 0609

Appendix A, The Significance Determination Process for Findings at Power, to assess

the significance of the finding. Per Exhibit 2, the finding represented a loss of function

for one train of Auxiliary Feedwater (AFW) for greater than the TS allowed outage time.

Therefore, the inspectors consulted the regional Senior Reactor Analyst for a detailed

risk evaluation. The inspectors considered the Unit 1 TDAFW pump inoperable since

the last successful surveillance on October 23, 2014. Given the evidence available, this

was the likely opportunity for the conditions to be established to set-up the improper

engagement between the TTV and the trip hook. In the detailed analysis, the finding

screened as Green, or very low safety significance. The finding had an associated

cross-cutting aspect in the area of human performance, specifically, H.8, Procedure

Adherence. During maintenance, work proceeded on the trip enclosure despite a lack of

detailed instructions on the removal/installation of the enclosure. (Section 1R19)

Cornerstone: Barrier Integrity

Green. The inspectors identified a non- violation of 10 CFR Part 50, Appendix B,

Criterion 3 Design Control, for the licensees inadequate radiological review of

permanently removing the Auxiliary Missile Blocks (AMBs) from the Unit 1 and Unit 2

5

containment accident shields. The finding was determined to be more than minor

because it was associated with the Barrier Integrity Cornerstone attribute of design

control; and adversely affected the cornerstone objective of maintaining radiological

barrier functionality of the safety-related accident shield. Specifically, the failure to

control plant design and adequately evaluate the radiological effects of permanently

removing the AMBs from the Unit 1 and Unit 2 containment accident shields did not

ensure that the accident shield will provide its design function to ensure safe radiation

levels outside the containment building following a maximum design basis accident.

The inspectors evaluated the finding using the Significance Determination Process

(SDP) in accordance with IMC 0609, Significance Determination Process, Attachment

0609.04, Initial Characterization of Findings, dated June 19, 2012. Because the finding

impacted the Barrier Integrity Cornerstone, the inspectors screened the finding through

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

dated June 19, 2012, using Exhibit 3, Barrier Integrity Screening Questions. The

finding screened as very-low safety significance (Green) because the finding only

represented a degradation of the radiological barrier function provided for the Auxiliary

Building. The inspectors determined the cause of this finding did not represent current

licensee performance and, thus, no cross-cutting aspect was assigned. (Section 1R18)

Cornerstone: Occupational Radiation Safety

Green. The inspectors identified a finding of very-low safety significance for inadequate

procedures used to verify Locked High Radiation Controls in the Unit 2 Containment with

an associated non- violation of TS 5.4, Procedures. As a result, weekly, from

November 1, 2013, to March 2014, multiple Radiation Protection Technicians verified the

Unit 2 Upper Containment Cavity Gate was locked; however it did not secure the area

against unauthorized access.

The inspectors determined that the performance deficiency was more than minor

because if left uncorrected the performance deficiency could lead to a more significant

safety concern. Specifically, the failure to identify deficient Locked High Radiation Area

(LHRA) controls could result in unintentional exposure to high levels of radiation. The

finding was determined to be of very-low safety significance because the problem was

not an as-low-as-is-reasonably-achievable (ALARA) planning issue, there was no

overexposure, nor substantial potential for an overexposure, and the licensees ability to

assess dose was not compromised. The inspectors did not identify a corresponding

cross-cutting aspect for this performance deficiency. The licensee entered the

deficiency in their Corrective Action Program as Action Request (AR) 2014-9001

immediately upon discovery and presentation by the inspectors. (Section 2RS1.1)

6

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period in a refueling outage. On October 29, 2014, the plant was

restored to 100 percent power. On November 1, rough lake conditions generated substantial

amounts of debris that clogged trash racks and travelling screens. The licensee manually

tripped the reactor and maintained the plant in hot standby (Mode 3). On November 8, the

licensee restored the plant to 100 percent power.

Unit 2 began the inspection period at 100 percent power. On November 1, 2014, rough lake

conditions generated substantial amounts of debris that clogged trash racks and travelling

screens. The licensee reduced power to 50 percent to reduce circulating water flow.

Conditions continued to degrade; therefore the licensee manually tripped the reactor. The

licensee cooled down and entered Mode 5 to repair an intermediate range nuclear instrument.

On November 13, the plant was restored to 100 percent power.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1

Winter Seasonal Readiness Preparations

a.

Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant specific design features and the licensees procedures used

to mitigate or respond to adverse weather conditions. Additionally, the inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR) and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant specific procedures. Cold weather protection, such as

heat tracing and area heaters, was verified to be in operation where applicable. The

inspectors also reviewed CAP items to verify that the licensee was identifying adverse

weather issues at an appropriate threshold and entering them into their CAP in

accordance with station corrective action procedures. Documents reviewed are listed in

the Attachment to this report. The inspectors reviews focused specifically on the

following plant systems due to their risk significance or susceptibility to cold weather

issues:

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b.

Findings

No findings were identified.

7

.2

Readiness for Impending Adverse Weather ConditionHigh Wind Conditions

a.

Inspection Scope

On November 6, 2014, the National Weather Service predicted high winds and rough

lake conditions in the vicinity of the plant. Since debris intrusion during similar conditions

the previous week had resulted in damage to equipment and a dual unit plant trip, the

inspectors validated the sites readiness for the adverse weather. The inspectors

reviewed the licensees overall preparations/protection for the expected weather

conditions. The inspectors walked down the service water screen house to assess the

licensee progress on repairing trash racks and traveling water screens. The inspectors

evaluated the licensee staffs preparations against the sites procedures and determined

that the staffs actions were adequate. During the inspection, the inspectors focused on

actions taken to minimize debris intrusion and operators preparations to address

degradation of raw water systems. The inspectors also reviewed a sample of CAP items

to verify that the licensee identified adverse weather issues at an appropriate threshold

and disposed them through the CAP in accordance with station corrective action

procedures. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one readiness for impending adverse weather condition

sample as defined in IP 71111.01-05.

b.

Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a.

Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Unit 2 Residual Heat Removal system after maintenance;

Unit 2 Steam Generator (SG) power-operated relief valves during maintenance

on other power-operated relief valves; and

Unit 2 AFW during maintenance on a single train.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, TS requirements, outstanding work orders (WOs), condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also walked down accessible

portions of the systems to verify system components and support equipment were

aligned correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

8

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment to this report.

These activities constituted three partial system walkdown samples as defined in

IP 71111.04-05.

b.

Findings

No findings were identified.

.2

Semiannual Complete System Walkdown

a.

Inspection Scope

On December 30, 2014, the inspectors completed a complete system alignment

inspection of the Unit 1 Containment Spray system to verify the functional capability of

the system. This system was selected because it was considered both safety significant

and risk significant in the licensees probabilistic risk assessment. The inspectors

walked down the system to review mechanical and electrical equipment lineups;

electrical power availability; system pressure and temperature indications, as

appropriate; component labeling; component lubrication; component and equipment

cooling; hangers and supports; operability of support systems; and to ensure that

ancillary equipment or debris did not interfere with equipment operation. A review of a

sample of past and outstanding WOs was performed to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the CAP database to ensure that system equipment alignment problems were

being identified and appropriately resolved. Documents reviewed are listed in the

Attachment to this report.

These activities constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b.

Findings

No findings were identified.

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

Unit 2 AB EDG;

Unit 2 CD EDG;

Unit 2 Quadrant cable tunnels; and

Unit 1 Essential Service Water Motor Control Center Room.

9

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources

within the plant, effectively maintained fire detection and suppression capability,

maintained passive fire protection features in good material condition, and implemented

adequate compensatory measures for out-of-service, degraded or inoperable fire

protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These activities constituted four quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b.

Findings

No findings were identified.

1R06 Flooding (71111.06)

.1

Underground Vaults

a.

Inspection Scope

The inspectors selected underground bunkers/manholes subject to flooding that

contained cables whose failure could disable risk-significant equipment. The inspectors

determined that the cables were not submerged, that splices were intact, and that

appropriate cable support structures were in place. In those areas where dewatering

devices were used, such as a sump pump, the device was operable and level alarm

circuits were set appropriately to ensure that the cables would not be submerged. In

those areas without dewatering devices, the inspectors verified that drainage of the area

was available, or that the cables were qualified for submergence conditions. The

inspectors also reviewed the licensees corrective action documents with respect to past

submerged cable issues identified in the corrective action program to verify the

adequacy of the corrective actions. The inspectors performed a walkdown of the

following underground bunkers/manholes subject to flooding:

Bunkers/manholes containing security cabling; and

Bunkers/manholes with safety-related cabling supporting technical specification

offsite power sources

Specific documents reviewed during this inspection are listed in the Attachment to this

report. This inspection constituted one underground vaults sample as defined in

IP 71111.06-05.

10

b.

Findings

No findings were identified.

1R07 Annual Heat Sink Performance (71111.07)

a.

Inspection Scope

The inspectors reviewed the licensees inspection of Unit 1 CD EDG north air aftercooler

to verify that potential deficiencies did not mask the licensees ability to detect degraded

performance, to identify any common cause issues that had the potential to increase

risk, and to ensure that the licensee was adequately addressing problems that could

result in initiating events that would cause an increase in risk. The inspectors observed

licensee visual observations of the internals of the heat exchanger to verify cleanliness

of the heat exchanger. Additionally, the inspectors reviewed eddy current testing results

and interviewed heat exchanger program engineers. Documents reviewed for this

inspection are listed in the Attachment to this document.

This annual heat sink performance inspection constituted one sample as defined in

IP 71111.07-05.

b.

Findings

No findings were identified.

1R08 Inservice Inspection Activities (71111.08P)

From September 29, 2014, through October 10, 2014, the inspector conducted a review

of the implementation of the licensees Inservice Inspection (ISI) Program for monitoring

degradation of the Unit 1 Reactor Coolant System (RCS), steam generator tubes,

Emergency Feedwater Systems, Risk Significant Piping and Components, and

Containment Systems.

The inspections described in Sections 1R08.1, 1R08.2, IR08.3, IR08.4, and 1R08.5

below constituted one inservice inspection sample as defined in IP 71111.08-05.

.1

Piping Systems Inservice Inspection

a.

Inspection Scope

The inspectors observed and reviewed records of the following non-destructive

examinations (NDE) mandated by the American Society of Mechanical Engineers

(ASME)Section XI Code to evaluate compliance with the ASME Code Section XI

and Section V requirements, and if any indications and defects were detected, to

determine whether these were dispositioned in accordance with the ASME Code or an

NRC-approved alternative requirement:

Ultrasonic (UT) examination of ASME Code Class 2, risk informed (R-A), pipe to

elbow weld, 1-FW-12-02S;

UT of ASME Code Class 1, Pressurizer Relief Nozzle inner Radius;

6-1-RC-7-IRS;

11

UT of ASME Code Class 1; Pressurizer Spray Nozzle Inner Radius;

4-1-RC-10-IRS; and

Magnetic Particle (MT) Examination of ASME Code Class 1, Pressurizer Vessel

Support; 1-PRZ-26.

There were no recordable indications identified during the previous refueling outage.

The inspectors reviewed NDE records associated with the following pressure boundary

welds completed for risk significant components during the current refueling outage to

determine whether the licensee applied the pre-service NDE and acceptance criteria

required by the Construction Code and ASME Code,Section XI. Additionally, the

inspectors reviewed the welding procedure specification and supporting weld procedure

qualification records to determine whether the weld procedure was qualified in

accordance with the requirements of Construction Code and the ASME Code Section IX:

Welds OW-1, OW-2 and OW-3 associated with replacement valve 1-CS-314

(Work Order 55440759-5); and

Welds OW-1 and OW-2 associated with replacement valve 1-NLI-112-V1 (Work

Order 55390312-01)

The inspectors also reviewed NDE records associated with the following pressure

boundary welds completed for risk significant systems since the beginning of the last

refueling:

Welds OW-1, 2, 3, 4, 5 and OW-6 associated with replacement of valve

1-NFP-222-V2 (Work Order 55421212-10/13); and

Welds OW-1 associated with the installation of pipe support 1-ARC-S4012

(WO Order 55404504-06).

b.

Findings

No findings were identified.

.2

Reactor Pressure Vessel Upper Head Penetration Inspection Activities

a.

Inspection Scope

For the Unit 1 reactor vessel head, no examination was required pursuant to

10 CFR 50.55a(g)(6)(ii)(D) for the current refueling outage. Therefore, no NRC review

was completed for this inspection procedure attribute.

b.

Findings

No findings were identified.

.3

Boric Acid Corrosion Control (BACC)

a.

Inspection Scope

The inspectors observed the licensees BACC visual examinations for portions of the

RCS, connected systems, and verified whether these visual examinations emphasized

12

locations where boric acid leaks can cause degradation of safety significant

components.

The inspectors reviewed the following licensee evaluations of RCS components with

Boric Acid deposits to determine whether degraded components were documented in

the corrective action system. The inspectors also evaluated corrective actions for any

degraded RCS components to determine whether they met the component Construction

Code, ASME Section XI Code, and/or NRC approved alternative:

AR 2013-4317; 1-QRV-114, body to bonnet leak;

AR 2013-4625;1-CS-448-1 has a BA leak;

AR 2013-5096; No. 14 SG cold leg nozzle dam leakage;

AR 2013-6839; U1C25 Refueling Cavity Leakage; and

AR 2013-7061; 1-RH-147W has Boric Acid on Body to Bonnet.

The inspectors reviewed the following corrective actions related to evidence of

BA leakage to determine whether the corrective actions completed were consistent with

the requirements of the ASME Code Section XI and 10 CFR Part 50, Appendix B,

Criterion XVI:

AR 2013-0534; 12-CS-185 has a body to bonnet leak;

AR 2014-9459; 12-CS-185 has a ruptured diaphragm;

AR 2013-7220; Reactor Head and Pressure Vent Piping Area;

AR 2013-7355; 1-NFP-240 has evidence of prior test fitting leakage; and

AR 2013-7067; 1-RH-107W leaks by at 0.095 ml/min.

b. Findings

No findings were identified.

.4

Steam Generator Tube Inspection Activities

a.

Inspection Scope

The NRC inspectors observed acquisition of eddy current (ET) data, interviewed ET data

analysts, and reviewed documentation related to the SG ISI Program to determine

whether:

the numbers and sizes of SG tube flaws/degradation identified was consistent

with the licensees previous outage Operational Assessment predictions;

the SG tube ET examination scope and expansion criteria were sufficient to meet

the Technical Specifications, and the Electric Power Research Institute (EPRI)

Document 1013706, Pressurized Water Reactor Steam Generator Examination

Guidelines;

the SG tube ET examination scope included potential areas of tube degradation

identified in prior outage SG tube inspections and/or as identified in NRC generic

industry operating experience applicable to these SG tubes;

the licensee-identified new tube degradation mechanisms and implemented

adequate extent of condition inspection scope and repairs for the new tube

degradation mechanism;

the licensee implemented qualified depth sizing methods to degraded tubes

accepted for continued service;

13

the ET probes and equipment configurations used to acquire data from the SG

tubes were qualified to detect the known/expected types of SG tube degradation

in accordance with Appendix H, Performance Demonstration for Eddy Current

Examination, of EPRI Document 1013706, Pressurized Water Reactor Steam

Generator Examination Guidelines;

the licensee performed secondary side SG inspections for location and removal

of foreign materials;

The licensee implemented repairs for SG tubes damaged by foreign material;

and

Foreign objects were left within the secondary side of the SGs, and if so, that the

licensee implemented evaluations, which included the effects of foreign object

migration and/or tube fretting damage.

b.

Findings

No findings were identified.

.5

Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI-related problems entered into the licensees

CAP and conducted interviews with licensee staff to determine whether:

the licensee had established an appropriate threshold for identifying ISI-related

problems;

the licensee had performed a root cause (if applicable) and taken appropriate

corrective actions; and

the licensee had evaluated operating experience and industry generic issues

related to ISI and pressure boundary integrity.

The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action

documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1

Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)

a.

Inspection Scope

On November 19, 2014, the inspectors observed a crew of licensed operators in the

plants simulator during licensed operator requalification training to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

licensed operator performance;

14

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

simulator sample as defined in IP 71111.11

b.

Findings

No findings were identified.

.2

Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)

a.

Inspection Scope

On October 17-18, 2014, the inspectors observed the drain-down and vacuum fill of the

RCS during the Unit 1 refueling outage. This was a high-risk (Orange) activity planned

during the outage. The inspectors evaluated the following areas:

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms (if applicable);

correct use and implementation of procedures;

control board (or equipment) manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications (if applicable).

The performance in these areas was compared to pre-established operator action

expectations, procedural compliance and task completion requirements. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk

sample as defined in IP 71111.11, and was done in conjunction with the requirements of

IP 71111.20.

15

1R12 Maintenance Effectiveness (71111.12)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

Nuclear Instrumentation;

Main Steam;

Anticipated Transient Without Scram Mitigating System Actuation Circuitry; and

Rod Position Indication

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

verifying appropriate performance criteria for SSCs/functions classified as (a)(2),

or appropriate and adequate goals and corrective actions for systems classified

as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted four quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b.

Findings

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

Rough lake conditions during emergent trash rack work;

Essential service water flow verification work concurrent with EDG testing; and

Emergent repairs to the Unit 2 Motor-Driven Auxiliary Feedwater (MDAFW) pump

room ventilation unit

16

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

Documents reviewed during this inspection are listed in the Attachment to this report.

These maintenance risk assessments and emergent work control activities constituted

three samples as defined in IP 71111.13-05.

b.

Findings

No findings were identified.

1R15 Operability Determinations and Functional Assessments (71111.15)

a.

Inspection Scope

The inspectors reviewed the following issues:

Main Steam Safety Valves lift during dual-unit trip;

Water intrusion into the Unit 1 TDAFW turbine bearings;

Question regarding TDAFW pump mission time;

Inability to make new ice during the Unit 1 refueling outage;

Inadvertent placement of FME bag on AB Fuel Oil Storage Tank vent;

Failure of automatic load tapping of Unit 2 Reserve Auxiliary Transformer and

failure of automatic generator trip during dual-unit trip; and

Leakby on a Unit 2 AFW flow control valve.

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted seven samples as defined in IP 71111.15-05.

17

b.

Findings

(1) Failure to Identify Conditions Adverse to Quality Associated with the Unit 1 TDAFW

Pump Turbine Oil System

Introduction: A finding of very low safety significance (Green) with an associated NCV of

10 CFR Part 50, Appendix B, Criterion 16, Corrective Actions, was identified by the

inspectors for the licensees failure to promptly identify and correct a CAQ associated

with Unit 1 TDAFW pump turbine bearing oil. Specifically, the licensee failed to identify

that water was entering the Unit 1 TDAFW pump turbine bearing oil system after leakage

had been identified directly above one of the TDAFW pump turbine bearings.

Description: On April 7, 2014, the licensee identified a 1 dpm leak from the Unit 1

TDAFW pump governor cooling pipe located directly above the outboard turbine bearing.

An AR was written (AR 2014-4473) which determined that due to the leak rate and the

apparent lack of any equipment impacts, there were no operability concerns. On

April 11, 2014, the licensee discovered that the turbine bearing oil level was

approximately 0.5 inches above the MAXIMUM mark on the sight glass. Level had been

recorded in the logs as being within band for over a year without any prior evidence of

high level. Additionally, there were no evolutions that had been performed which would

explain the high level. The licensee generated AR 2014-4684 to document this

condition. The AR documented several possible reasons for the unexplained level rise.

One was that turbine building temperature had gone up. Another was that it was not

uncommon for personnel to unnecessarily add oil to the machine from time to time. No

other information was provided to validate either potential cause. Additionally, there was

no mention of the leak identified above one of the turbine bearings four days prior. No

formal monitoring plan was established. An action was created to sample the oil for

water, but as of six weeks later, a work order had not been finalized and scheduled.

The only other action was a lessons-learned that was created for Mechanical

Maintenance department regarding unnecessary oil adds. The response to the action

from the group was that they dont typically do oil adds, but that they discussed the topic

anyway. The inspectors reviewed reference information with respect to oil levels and

their importance to machine operability. According to the vendor manual, EPRI

guidance on Terry turbines, and an AR the licensee evaluated in 2012, oil level is

extremely critical in the turbine bearing pedestals. The references all concluded that oil

level above the MAXIMUM mark could lead to oil frothing, which could affect stable

operation of the turbine and loss of oil from the system. Further, the references, along

with the plant logs, stated that oil level should be kept at or slightly above the MINIMUM

mark. Action Request 2014-4684 concluded that in April 2013, the reservoir was

over-filled to the MAXIMUM mark. No further information was provided on why this

occurred or why it was acceptable to stay at the MAXIMUM mark. One quart of oil was

drained from the turbine bearing pedestals, bringing the level back to near the

MAXIMUM mark. Approximately five weeks later, an NRC inspector touring the plant

questioned why level was near the MAXIMUM mark given a placard near the sight glass

said to keep level at the MINIMUM mark (which aligned with the references above).

The licensee generated an AR (2014-6315) about one week later on May 22 when the

inspector asked about the condition again. In the AR, they documented the NRC

observation and also the fact that an operator had noted level to be above the

MAXIMUM mark by approximately 0.25 inches. Oil was again drained from the

machine, this time to right above the MINIMUM mark. The operability assessment

(which was not documented until the following day), stated that at time of discovery, the

18

machine was operable because of oil level not affecting operability of the turbine and a

history of overfilling that sometimes required draining of the oil. Further, a statement

was made that there had been a consistent oil level trend for the past month. Again,

the leakage above the bearing was not discussed. There was no discussion of the

previous high-level condition from April 11. On May 23, the licensee decided to

completely drain the oil and sample it for water; 620 ml of water was found in the 2.5

gallon system. New oil was added, and an apparent cause evaluation was performed.

The evaluation concluded that leakage above the bearing housing (documented

originally in AR 2014-4473), combined with a small casing steam leak that condensed

above the housing while the machine was in operation, caused the water intrusion in the

bearing oil. Later evaluation determined the leak rate from the pipe had increased to

8 dpm in standby, and while running the leak rate was 20 dpm. The leakage sources

were diverted away from the bearing housing with a temporary modification pending

repairs (which were completed in the September-October 2014 refueling outage).

Based on the above, the inspectors concluded the licensee had sufficient information to

promptly identify and correct water intrusion into the TDAFW turbine bearing oil system

on April 11 and May 22, 2014. Additionally, the licensee failed to identify the potential

operability impacts (as described in the multiple references above) on April 11 and

May 22 when oil level was above the MAXIMUM mark. Water intrusion into safety-

related oil systems is a CAQ.

Analysis: The failure to promptly identify and correct a CAQ, as required by

10 CFR Part 50, Appendix B, Criterion 16, associated with water intrusion into the

TDAFW turbine oil system was an issue warranting further review in the SDP. Per

IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, the issue was

more-than-minor because it adversely affected the Configuration Control attribute of the

Mitigating Systems Cornerstone, whose objective is to ensure the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences. Additionally, if left uncorrected, the issue could lead to a more significant

safety concern. Specifically, not recognizing water intrusion into safety-related oil

systems can impact operability and affect how safety equipment operates.

The inspectors assessed the finding for significance using IMC 0609, Significance

Determination Process, issued June 2, 2012. Per Appendix A, The Significance

Determination Process (SDP) for Findings-at-Power, issued June 19, 2012, the finding

screened as Green, or very low safety significance, in Exhibit 2. Specifically, all

questions were answered no under Section A for findings related to Mitigating SSCs

and Functionality. The inspectors reviewed the licensees past operability evaluation

and concluded that given the projected amount of water that could be entrained in the oil

during operation, along with the duration of operation assumed in the safety analyses,

that operability of the pump would be maintained.

The inspectors determined the finding had an associated cross-cutting aspect in the

Human Performance area, specifically, H.11, Challenge the Unknown. Some of the

tenets of H.11, as described in NUREG-2165, Safety Culture Common Language

Initiative, Section QA.2, Questioning Attitude, are that individuals avoid complacency

and continuously challenge existing conditions in order to identify discrepancies that

might result in error or inappropriate action. Further, it states that individuals challenge

unanticipated results rather than rationalize them, and that abnormal indications are not

attributed to indication problems. Regarding the TDAFW oil system, the licensee

rationalized why the level was increasing without sufficient investigation given the

19

significance of the system, and did not seek further information that was readily available

regarding appropriate oil levels.

Enforcement: 10 CFR Part 50, Appendix B, Criterion 16, Corrective Action, requires, in

part, that conditions adverse to quality, such as deficiencies, defective material and

equipment, and nonconformances are promptly identified and corrected.

Contrary to the above, between April 11 and May 23, 2014, the licensee failed to

promptly identify and correct a CAQ. Specifically, the licensee failed to promptly identify

and correct water intrusion into the safety-related Unit 1 TDAFW pump oil system

despite multiple opportunities to do so. On April 7, the licensee became aware of a

water leak directly above the TDAFW pump turbine outboard bearing. On April 11, and

May 22, the licensee learned that the oil level had exceeded the MAXIMUM mark. The

actions taken (draining the oil level) did not correct the condition adverse to quality in

that water continued to leak into the oil. On May 23, the licensee drained the oil system

and discovered approximately 620 ml of water.

For immediate corrective actions, the licensee added new oil to the system and installed

a temporary modification to prevent further water intrusion. Further corrective actions

included an apparent cause evaluation and past operability evaluation. Permanent

repairs to the cooling water leak above the bearing were completed during the Fall 2014

refueling outage. The licensee initiated AR-2014-6315 to document the condition and

track corrective actions.

This violation is being treated as an NCV, consistent with Section 2.3.2 of the

Enforcement Policy because it was of very low safety significance and was entered into

the licensees CAP. (NCV 05000315/2014005-01; Failure to Identify Conditions

Adverse to Quality associated with the Unit 1 TDAFW Pump Turbine Oil System)

(2) Unplanned Inoperability of the AB Fuel Oil Storage Tank During Maintenance

Introduction: A finding of very low safety significance (Green) with an associated NCV of

TS 5.4, Procedures, was self-revealed when a vacuum was inadvertently drawn on the

AB FOST during preparations for surveillance activities. The vacuum caused an

indication of lowering level in the tank, alarms, and an unplanned TS LCO action

statement entry.

Description: On August 20, 2014, the licensee was performing work activities in

preparation for an upcoming, routine leak-test of the AB FOST. The AB FOST is one of

two underground tanks on site that supply fuel to the EDGs via the smaller day tanks

(which are provided for each EDG and offer a more limited, immediate fuel supply). The

test consists of establishing a vacuum in the tank and monitoring it for a period of time.

Several support activities are required to be performed prior to the test, some of which

include transfer of fuel from the FOST to the day tanks, removal of a vent cover for the

FOST, and connection of vendor-supplied vacuum and test equipment to the vent. Per

the overarching surveillance procedure, the basic order of activities should have been to

loosen the vent cover, transfer an amount of fuel to the day tanks, remove the FOST

from service, remove the vent cover, hook up the test equipment, and perform the test.

During the day shift on August 20, workers went out to work on the vent cover. The

associated work instruction did not provide adequate guidance on what exactly was to

be done. While the intent was just to loosen the cover at that point, the Subject of the

20

WO was Remove manway cover and vent cover. The instructions in the WO were

written as loosen/remove vent cover, and under the Precautions section the statement

Per tank procedure, as a minimum, we only have to loosen vent filter. The workers

ended up removing the cover instead of loosening it, and placed an FME bag over the

vent to prevent foreign material from entering the tank. Later on night shift, operations

staff commenced the transfer of fuel to the day tanks. With the FME bag installed, a

vacuum was drawn on the tank. Based on the configuration of the level instruments and

tank vent, the instruments indicated a lowering tank level and generated low level alarms

because of the vacuum. Operators performed a back-up measurement of tank level

using a dip stick, however, again, based on the tank construction, this method also

showed what appeared to be a lowering tank level. With this information, operators

believed an actual loss of fuel from the tank had occurred. Absent any indications in the

plant of fuel leaving the system, they concluded a release to the environment may have

occurred. Appropriate reports were made to state, federal, and local agencies.

Additionally, the operators entered TS LCO 3.8.3 Condition A based on the observed

level indications. During investigation soon after the abnormal level indications, the FME

bag was found on the vent. Once removed, level in the tank returned to normal. There

was no actual loss of fuel from the tank.

Analysis: The failure to have adequate instructions for performing work on safety-related

equipment, as required by TS 5.4, Procedures, was a performance deficiency

warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued

September 7, 2012. The performance deficiency was more than minor because it

adversely impacted the Configuration Control attribute of the Mitigating Systems

cornerstone, whose objective is ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

The finding screened as Green, or very low safety significance, utilizing IMC 0609

Appendix A, The Significance Determination Process for Findings at Power, issued

June 19, 2012. Specifically, all questions were answered no under Section A of

Exhibit 2 for Mitigating Systems, since that was the affected cornerstone. The FME bag

was installed, which rendered the AB FOST inoperable, for approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

This was less than the TS allowed outage time of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

The finding had an associated cross-cutting aspect in the human performance area,

specifically, H.5, Work Management. Work activities should be planned, controlled, and

executed with nuclear safety as the overriding priority. Contrary to the tenets of the

cross-cutting aspect, the work was planned and executed with inadequate work

instructions. Further, there was a lack of coordination between a number of work groups

and activities associated with the test.

Enforcement: Technical Specification 5.4, Procedures, states, in part, that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in

part, that maintenance that can affect the performance of safety-related equipment

should be properly preplanned and performed in accordance with written procedures,

documented instructions, or drawings appropriate to the circumstances.

Contrary to those requirements, on August 20, 2014, the AB FOST leak test was

performed with inadequate procedures and with tasks done outside the proper

21

sequence. As a result, the AB FOST was rendered inoperable for approximately

16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />.

Immediate corrective actions involved the removal of an FME bag which had been

placed over the AB FOST vent. The licensee also generated AR-2014-9877, which

included a root cause analysis. This violation is being treated as an NCV, consistent

with Section 2.3.2 of the Enforcement Policy because it was of very low safety

significance and was entered into the licensees CAP. (NCV 05000315/2014005-02; 05000316/2014005-02; Unplanned Inoperability of the AB Fuel Oil Storage Tank

During Maintenance)

1R18 Plant Modifications (71111.18)

a.

Inspection Scope

The inspectors reviewed the following modification(s):

Permanent removal of shield/missile blocks

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety

evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to

verify that the modification did not affect the operability or availability of the affected

system(s). The inspectors, as applicable, observed ongoing and completed work

activities to ensure that the modifications were installed as directed and consistent with

the design control documents; the modifications operated as expected; post-modification

testing adequately demonstrated continued system operability, availability, and reliability;

and that operation of the modifications did not impact the operability of any interfacing

systems. As applicable, the inspectors verified that relevant procedure, design, and

licensing documents were properly updated. Lastly, the inspectors discussed the plant

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how the operation with the plant modification in place could

impact overall plant performance. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted one permanent plant modification sample as defined in

IP 71111.18-05.

b.

Findings

Lack of Adequate Design Review of Effects of Removing the Auxiliary Missile Blocks

from the Containment Accident Shield

Introduction: A finding of very-low safety significance (Green) and associated NCV of

Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, was identified by the

NRC inspectors for the licensees inadequate radiological review of permanently

removing the AMBs from the Unit 1 and Unit 2 containment accident shields.

Description: In March 2014, the NRC reviewed a licensee modification

(EC-0000049191) to the Unit 1 and 2 safety-related containment accident shields. The

modification consisted of permanently removing the AMBs, located in front of the primary

containment equipment hatches on the 650 elevation of the Auxiliary Building. The

AMBs are portable and removable shield blocks and are a part of the safety-related

22

containment accident shield. The AMBs are in place during power operations for

shielding purposes. The AMBs are removed during plant outages to permit containment

access for equipment.

The main purpose of the accident shield, as a part of original plant design and currently

described in the UFSAR, Section 11.2.1.1.4, is to ensure safe radiation levels outside

the containment building following a maximum design-basis accident; specifically, a

large break loss-of-coolant accident (LBLOCA). The plant containment and the accident

shield function (USFAR Section 11.2.1) ensure that operating personnel at the plant and

the general public are protected by adequate containment shielding, post LBLOCA. This

was in accordance with plant specific design Criteria 1 of 10 CFR Part 50 General

Design Criteria 1 Quality Standards and Records of Appendix A General Design

Criteria for Nuclear Power Plants, 10 CFR Part 20 Standards for Protection Against

Radiation, and 10 CFR Part 100 Reactor Site Criteria. The inspectors reviewed the

original and current plant design configuration and determined that, prior to plant

modification (EC-0000049191), the plant design met General Design Criteria 1 for

radiation safety. Specifically, RG 1.69 Concrete Radiation Shields for Nuclear Power

Plants was explicit in stating that General Design Criteria 1 for containment ensures

reasonable assurance for compliance to 10 CFR Part 20 Standards for Protection

Against Radiation under post-accident conditions. Additionally, initial plant design for

the containment accident shield was consistent with RG 1.69 Concrete Radiation

Shields for Nuclear Power Plants.

Using the licensees design basis source term, licensee calculation number RS-C-0046

Doses and Dose Rates from Post LOCA Airborne Sources determined that with the

AMBs in place, the Post LBLOCA dose rates were:

A nominal 31 Rem/hr at 1 second after LBLOCA at 1 inch from the AMBs; and

A nominal 3.9 Rem/hr at 1 second after LBLOCA at 50 feet from the AMBs.

These dose rates provide for safe radiation levels outside the containment building

following a maximum design-basis accident consistent with the UFSAR design

statements and in accordance with the requirements of 10 CFR Part 20, Standards for

Protection Against Radiation.

The licensee provided no comparable post-modification dose rate calculations to the

inspectors specific to AB 650 elevation once the AMBs were removed. However, the

licensee provided information (Calculation Number RS-C-0232, Equipment Hatch Dose

Rates - Gap Release; Revision 01) that showed calculated Post LBLOCA dose rates

of 196.2 Rem/hr at 45 feet from the equipment hatch. Additionally, the licensee had

analogous Post-LBLOCA dose rate calculations for the containment personnel hatch.

These dose rates provide a frame of reference, in that, the calculations provide for no

AMB shielding. However, the calculations did include shielding benefit from the inside

containment crane wall (Calculation Number RS-C-0046, Doses and Dose Rates from

Post LOCA Airborne Sources). Specific calculated dose rates were:

A nominal 36,300 Rem/hr at 1 second after LBLOCA at 1 inch from the personnel

hatch; and

A nominal 397 Rem/hr at 1 second after LBLOCA at 50 feet from the personnel

hatch.

23

The inspectors determined that post-modification dose rates on the AB 650 elevation

could result in lethal doses, as defined in NUREG/CR 6545 Probabilistic Accident

Consequence Uncertainty Analysis: Early Health Effects Uncertainty Assessment, to

individuals in a very short period of time (from fractions of a second to minutes,

depending on the location of personnel relative to the radiation source). By permanently

removing the AMBs, the licensee failed to provide for safe radiation levels outside the

containment building following a maximum design-basis accident, contrary to the design

bases and inconsistent with the requirements of 10 CFR Part 20.

Additionally, 10 CFR 20.1101(b) and RG 1.69 state, in part, that the licensee shall use,

to the extent practical, engineering controls based upon sound radiation principles to

achieve occupational doses and doses to members of the public that are

as-low-as-reasonably-achievable (ALARA). Original plant design and the plants 40-year

operational history demonstrate that plant operation with the AMBs in place was both

practical and ALARA.

The licensee documented this issue in the CAP as AR 2014-13016. Corrective actions

included licensee determination to achieve radiation attenuation analogous to original

plant design of the AMBs in place.

Analysis: The inspectors determined that the licensees inadequate radiological review

of permanently removing the AMBs from the Unit 1 and Unit 2 containment accident

shields was a performance deficiency. The performance deficiency was determined to

be more than minor (Green) because it was associated with the Barrier Integrity

Cornerstone attribute of design control; and adversely affected the cornerstone objective

of maintaining radiological barrier functionality of the safety-related containment accident

shield. Specifically, the failure to control plant design and adequately evaluate the

radiological effects of permanently removing the AMBs from the Unit 1 and Unit 2

containment accident shields did not ensure that the accident shield will provide its

design function to ensure safe radiation levels outside the containment building following

a maximum design basis accident.

The inspectors evaluated the finding using the SDP in accordance with IMC 0609,

Significance Determination Process, Attachment 0609.04, Initial Characterization of

Findings, dated June 19, 2012. Because the finding impacted the Barrier Integrity

Cornerstone, the inspectors screened the finding through IMC 0609, Appendix A, The

Significance Determination Process for Findings At-Power, dated June 19, 2012, using

Exhibit 3, Barrier Integrity Screening Questions. The finding screened as of very-low

safety significance (Green) because the finding only represented a degradation of the

radiological barrier function provided for the Auxiliary Building.

The inspectors determined the cause of this finding did not represent current licensee

performance and, thus, no cross-cutting aspect was assigned.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion 3, Design Control, requires,

in part, that design changes be subject to design control measures commensurate with

those applied to the original design.

Contrary to the above, on February 6, 2009, the licensee performed a design change

and failed to subject it to design control measures commensurate with those applied to

the original design. Specifically, the licensee modified the original plant design by

24

removing the auxiliary missile blocks from the safety-related accident shield. However,

the design control measures applied to the modification failed to ensure safe radiation

levels outside the containment accident shield following a design basis loss-of-coolant

accident.

Because this violation was of very-low safety significance and was entered into the

licensees CAP (AR 2014-13016), this violation is being treated as an NCV, consistent

with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000315/2014005-03; 05000316/2014005-03; Radiological Impact of the Removal of the Auxiliary Shield

Blocks on the Containment Accident Shield Post LBLOCA)

1R19 Post-Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

Unit 1 AB EDG following governor replacement;

Unit 1 CRID III and IV maintenance;

Unit 2 UAT breakers following failure to close;

Unit 1 CD EDG governor replacement and aftercooler maintenance;

Unit 1 TDAFW governor overhaul;

Repair of Unit 2 AFW flow control valve flow retention issue;

Repair of circuitry associated with failure of fast transfer and generator trip during

dual-unit trip; and

Unit 1 TDAFW repairs following inadvertent trip.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted eight post-maintenance testing samples as defined in

IP 71111.19-05.

25

b.

Findings

Introduction: A finding of very low safety significance (Green) with an associated NCV of

TS 5.4, Procedures, was self-revealed on November 1, 2014, when the Unit 1 TDAFW

pump tripped during an emergent dual-unit shutdown. Both units were taken offline by

operators due to debris intrusion from Lake Michigan into the cooling water

screenhouse. The TDAFW pump started as expected but shutdown after a few minutes

of operation.

Description: On November 1, 2014, operators removed both units from service in

response to excessive debris intrusion into the cooling water screenhouse. Following

the trip of both reactors, AFW pumps started as expected. However, the Unit 1 TDAFW

unexpectedly turned off after a few minutes of operation while operators were adjusting

flow to the steam generators. Adequate flow continued to be provided by the two other

AFW pumps. During the ensuing forced outage to address the debris intrusion issue,

the licensee performed an investigation into why the pump tripped off. The licensee

explored and ruled out causes such as a pump overspeed, failed overspeed trip circuitry,

and governor control problems. The investigation included several test runs of the pump

while rapidly changing demand in an effort to stress the pump and replicate the trip

event. During continued troubleshooting, the licensee later discovered a protective

enclosure around an electronic component (the trip solenoid) had been installed

incorrectly. The enclosure was relatively loose, and the licensee found by moving it

slightly, it could be placed in a position where a threaded rod on the enclosure could

interfere with the proper latching of the TTV for the pump. When the pump turns on, the

TTV opens to admit steam to the turbine. As the valve stem moves up, an attachment

engages a trip hook. The trip hook basically acts to hold the valve open. On a trip

condition, such as a pump overspeed, the hook would move out of the way, allowing the

valve to shut and the pump to turn off. Precise engagement between the TTV and the

trip hook is required for the pump to operate correctly. In this case, the licensees

apparent cause evaluation determined the most likely cause was inadequate trip hook

engagement as a result of the interference from the trip solenoid enclosure. As part of

the extent-of-condition, the licensee discovered the same potential issue on the Unit 2

TDAFW pump. Further investigation revealed that the enclosure was not captured in

design diagrams, and that work instructions regarding its installation/removal were not

detailed. Most recently, the Unit 1 TDAFW pump trip solenoid enclosure had been

removed and reinstalled during the Fall 2014 refueling outage as part of planned

maintenance. Working with the pump vendor, the licensee identified the correct

configuration of the enclosure and reinstalled them correctly on both pumps. The

licensee tested the pump several times afterwards, and restored the Unit 1 TDAFW

pump to operable status at the conclusion of the forced outage.

Analysis: The failure to have adequate instructions for performing work on safety-related

equipment, as required by TS 5.4, Procedures, was a performance deficiency

warranting further review utilizing IMC 0612, Appendix B, Issue Screening, issued

September 7, 2012. The performance deficiency was more than minor because it

adversely impacted the Configuration Control attribute of the Mitigating Systems

cornerstone, whose objective is ensuring the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

The inspectors utilized IMC 0609 Appendix A, The Significance Determination Process

for Findings at Power, issued June 19, 2012, to assess the significance of the finding.

26

Per Exhibit 2, the finding represented a loss of function for one train of AFW for greater

than the TS allowed outage time. Therefore, the inspectors consulted the regional

Senior Reactor Analyst (SRA) for a detailed risk evaluation. The inspectors considered

the Unit 1 TDAFW pump inoperable since the last successful surveillance on

October 23. Given the evidence available, this was the likely opportunity for the

conditions to be established to set-up the improper engagement between the TTV and

the trip hook.

The Region III SRA used the NRC standardized plant analysis risk model for D.C. Cook

to perform a detailed risk evaluation. The model has internal and external event

initiators. The SRA assumed an exposure period for the condition of 9 days. The delta

core damage frequency (CDF) calculated was 4.5E-7/yr, which is a finding of very low

safety significance (Green). The dominant risk sequence was a fire in the turbine

building, followed by a failure of main feedwater, auxiliary feedwater and feed and bleed.

Since the calculated delta CDF was greater than 1E-7/yr, the SRA also considered the

potential impact of the finding on large early release frequency using IMC 0609

Appendix H, Containment Integrity Significance Determination Process. The plant has

an ice condenser containment and sequences important to large early release frequency

are steam generator tube rupture, inter-system loss-of-coolant accident, and station

blackout. Some of the sequences that contributed to the change in CDF included station

blackout sequences but their contribution was less than 1E-7/yr. The SRA concluded

that the risk of this finding should be characterized by the overall change in CDF.

The finding had an associated cross-cutting aspect in the area of human performance,

specifically, H.8, Procedure Adherence. Safety Culture Common Language Initiative

NUREG-2165 provides an example of the aspect as individuals review procedures

before work to validate they are appropriate for scope of work, and ensure required

changes are completed before implementation. Contrary to this description, work

proceeded on the trip enclosure despite a lack of detailed instructions on the

removal/installation of the enclosure.

Enforcement: Technical Specification 5.4, Procedures, states, in part, that written

procedures shall be established, implemented, and maintained covering the applicable

procedures recommended in Regulatory Guide 1.33. Regulatory Guide 1.33 states, in

part, that maintenance that can affect the performance of safety-related equipment

should be properly preplanned and performed in accordance with written procedures,

documented instructions, or drawings appropriate to the circumstances.

Contrary to those requirements, work was performed on the Unit 1 TDAFW pump trip

solenoid enclosure with inadequate work instructions. As a result, an apparent cause

evaluation determined the misplaced enclosure was the likely cause of the pump

failure during an actual demand following a dual-unit trip. The violation existed from

October 23, 2014, until troubleshooting and post-maintenance testing activities were

completed on November 3, 2014, following the dual-unit trip.

For immediate corrective actions, the licensee initiated AR-2014-13668 and began

troubleshooting activities. The licensee investigation revealed the misplaced trip

solenoid enclosure to be the likely cause of the pump trip. Subsequently, the enclosures

were installed in the correct position. This violation is being treated as an NCV,

consistent with Section 2.3.2 of the Enforcement Policy because it was of very low safety

27

significance and was entered into the licensees CAP. (NCV 05000315/2014005-04;

Inadvertent Trip of the Unit 1 TDAFW Pump)

1R20 Outage Activities (71111.20)

.1

Refueling Outage Activities

a.

Inspection Scope

The inspectors reviewed the Outage Safety Plan and contingency plans for the Unit 1

refueling outage, conducted September 24 - October 24, 2014, to confirm that the

licensee had appropriately considered risk, industry experience, and previous

site-specific problems in developing and implementing a plan that assured maintenance

of defense-in-depth. During the refueling outage, the inspectors observed portions of

the shutdown and cooldown processes and monitored licensee controls over the outage

activities listed below:

licensee configuration management, including maintenance of defense-in-depth

commensurate with the Outage Safety Plan for key safety functions and

compliance with the applicable TS when taking equipment out of service;

implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing;

installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication, accounting for instrument error;

controls over the status and configuration of electrical systems to ensure that

TS and Outage Safety Plan requirements were met, and controls over switchyard

activities;

monitoring of decay heat removal processes, systems, and components;

controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system;

reactor water inventory controls including flow paths, configurations, and

alternative means for inventory addition, and controls to prevent inventory loss;

controls over activities that could affect reactivity;

maintenance of secondary containment as required by TS;

licensee fatigue management, as required by 10 CFR 26, Subpart I;

refueling activities, including fuel handling and sipping to detect fuel assembly

leakage;

startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the drywell (primary containment) to verify that debris had not been

left which could block emergency core cooling system suction strainers, and

reactor physics testing; and

licensee identification and resolution of problems related to refueling outage

activities.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one Refueling Outage sample as defined in IP 71111.20-05.

28

b.

Findings

No findings were identified.

.2

Unit 1 and Unit 2 Forced Outages Commencing November 1, 2014

a.

Inspection Scope

On November 1, rough lake conditions generated substantial amounts of debris that

clogged trash racks and travelling screens. The licensee manually tripped the Unit 1

reactor and initially reduced power to 50 percent on the Unit 2 reactor to reduce

circulating water flow. Conditions continued to degrade; therefore the licensee

subsequently tripped the Unit 2 reactor. Unit 1 remained in Mode 3 and returned to

100 percent power on November 8. Unit 2 was cooled down to Mode 5 to repair an

intermediate range nuclear instrument. Unit 2 was returned to 100 percent power on

November 13. The inspectors toured portions of containment, observed shutdown and

startup activities, assessed plant risk, and observed maintenance activities.

This inspection constituted one Forced Outage sample as defined in IP 71111.20-05.

b.

Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

1-OHP-4030-108-008R, Unit 1 ECCS Check Valve Test, (IST);

1-EHP-4030-134-203, Unit 1 LLRT (Containment Isolation Valve);

12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance,

(Ice Condenser Surveillance);

Unit 1 Control Room Emergency Ventilation Surveillance, 1-EHP-4030-128-229

(Routine); and

Loss of Offsite Power/Loss-of-Coolant Accident Circuit Testing (Routine).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

did preconditioning occur;

the effects of the testing were adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the USAR, procedures, and applicable commitments;

29

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers code, and reference values were consistent with the

system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two routine surveillance testing samples, one inservice

testing sample, one ice condenser surveillance, and one containment isolation valve

sample as defined in IP 71111.22, Sections-02 and-05.

b.

Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

The regional inspectors performed an in-office review of the latest revisions to the

Emergency Plan and Emergency Plan Implementing Procedures as listed in the

Attachment to this report.

The licensee transmitted the Emergency Plan and Emergency Action Level revisions to

the NRC pursuant to the requirements of 10 CFR Part 50, Appendix E, Section V,

Implementing Procedures. The NRC review was not documented in a safety

evaluation report and did not constitute approval of licensee-generated changes;

therefore, this revision is subject to future inspection. The specific documents reviewed

during this inspection are listed in the Attachment to this report.

30

This Emergency Action Level and Emergency Plan Change inspection constituted one

sample as defined in IP 71114.04-06.

b.

Findings

Introduction: An Unresolved Item (URI) was identified because additional information is

required to determine whether a performance deficiency that is more than minor exists

and if a violation of 10 CFR 50.54(q)(3) occurred. The inspectors identified an issue of

concern for a change to the Donald C. Cook Emergency Plan, Table 1, that reduced the

number of Radiation Protection Technicians (RPTs) required to augment the on-shift

emergency response organization in 60 minutes of a declared emergency and replaced

them with a Radiological Assessment Coordinator (RAC) and an Environmental

Assessment Coordinator (EAC).

Description. During the review, the inspectors identified a change made in Table 1 of

Revision 35 to the Emergency-Plan (E-Plan), dated June 3, 2014. The change reduced

the number of 60-minute response RPTs tasked with conducting offsite surveys from

three RPTs to two RPTs and one EAC. The second change reduced the number of

60-minute response RPTs tasked with conducting in-plant surveys from two RPTs to one

RPT and one RAC. According the licensees 10 CFR 2014 50.54(q) screening

evaluation, this change was to align the wording in Table 1 with Sections B.5.a.4 and

B.5.c.4 of the E-Plan. The inspectors identified that the wording in Section B.5.a.4 and

B.5.c.4 of the E-Plan had been changed to include the EAC and the RAC as 60-minute

responders in Revision 19 of the plan in March of 2004. Inspectors review of the

10 CFR 50.54(q) screening for the changes in Revision 19, identified no evaluations had

been done for this change. The inspectors reviewed Revision 18 of the E-Plan and the

associated March 21, 2003 licensee request for prior approval for changes to the E-plan

that was conducted, approved by the NRC, and implemented in this revision. The NRC

approved change request included specific numbers of RPTs for 60-minute response

tasks of three RPTs for offsite surveys and 2 RPTs for onsite surveys.

The licensee indicated that the EAC and RAC were not currently qualified RPTs. This

suggests a performance deficiency, due to the appearance of a reduction in

effectiveness to the licensees E-plan, without prior NRC approval. However, in order to

determine if this is a performance deficiency of more than minor significance, additional

information is required to understand if the RAC and EAC positions had equivalent

capabilities as the qualified RPTs. The licensee has entered this issue in their

Corrective Action Program as AR 2014-15685, Potential EP Finding. Compensatory

actions were taken while their staff gathers additional information, which included

requiring two additional qualified RPTs to respond to the Operations Support Center

within 60 minutes prior to activating the facility in the event of a declared emergency.

The licensee stated that it will provide the inspectors with additional information within

30 days of the exit meeting.

Therefore, a URI was identified pending additional information. Specifically,

documentation demonstrating the knowledge, skills, and abilities of the EAC and RAC

are equivalent to the RPTs is necessary for the inspectors to determine whether the

performance deficiency is more than minor and if a violation of 10 CFR 50.54(q)

occurred. (URI 05000315/2014005-05; Changes to Minimum 60-Minute Emergency

Responder Staffing Without Prior Approval)

31

2.

RADIATION SAFETY

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

The inspection activities supplement those documented in NRC Inspection Report

05000315-05000316/2014002 and constitute one complete sample as defined in

Inspection Procedure 71124.01-05.

.1

Radiological Hazard Assessment (02.02)

a.

Inspection Scope

The inspectors determined whether there have been changes to plant operations since

the last inspection that may result in a significant new radiological hazard for onsite

workers or members of the public. The inspectors evaluated whether the licensee

assessed the potential impact of these changes and has implemented periodic

monitoring, as appropriate, to detect and quantify the radiological hazard.

The inspectors reviewed the last two radiological surveys from selected plant areas and

evaluated whether the thoroughness and frequency of the surveys where appropriate for

the given radiological hazard.

The inspectors selected the following radiologically risk significant work activities that

involved exposure to radiation:

Refuel Cavity Decontamination Activities;

Steam Generator Platform Activities;

Valve Maintenance / Repair;

Perform Radiography in Auxiliary and Turbine Buildings and Plant Restricted

Areas; and

Reactor Pit Very High Radiation Area (VHRA) Downpost Survey.

For these work activities, the inspectors assessed whether the pre-work surveys

performed were appropriate to identify and quantify the radiological hazard and to

establish adequate protective measures. The inspectors evaluated the radiological

survey program to determine if hazards were properly identified, including the following:

identification of hot particles;

the presence of alpha emitters;

the potential for airborne radioactive materials, including the potential presence

of transuranics and/or other hard-to-detect radioactive materials (This evaluation

may include licensee planned entry into non-routinely entered areas subject to

previous contamination from failed fuel.);

the hazards associated with work activities that could suddenly and severely

increase radiological conditions and that the licensee has established a means to

inform workers of changes that could significantly impact their occupational dose;

and

severe radiation field dose gradients that can result in non-uniform exposures of

the body.

32

The inspectors observed work in potential airborne areas and evaluated whether the air

samples were representative of the breathing air zone. The inspectors evaluated

whether continuous air monitors were located in areas with low background to minimize

false alarms and were representative of actual work areas. The inspectors evaluated

the licensees program for monitoring levels of loose surface contamination in areas of

the plant with the potential for the contamination to become airborne.

b.

Findings

No findings were identified.

.2

Instructions to Workers (02.03)

a.

Inspection Scope

The inspectors reviewed the following radiation work permits used to access high

radiation areas and evaluated the specified work control instructions or control barriers:

RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;

RWP 141148; U1C26 - Steam Generator Platform Activities;

RWP 141145; U1C26 - Valve Maintenance / Repair;

RWP 1 41130; U1C26 - Perform Radiography in Auxiliary & Turbine Buildings &

Plant Restricted Areas; and

RWP 141172; U1C26 - Reactor Pit VHRA Downpost Survey.

For these radiation work permits, the inspectors assessed whether allowable stay times

or permissible dose (including from the intake of radioactive material) for radiologically

significant work under each radiation work permit were clearly identified. The inspectors

evaluated whether electronic personal dosimeter alarm set-points were in conformance

with survey indications and plant policy.

For work activities that could suddenly and severely increase radiological conditions, the

inspectors assessed the licensees means to inform workers of changes that could

significantly impact their occupational dose.

b.

Findings

No findings were identified.

.3

Contamination and Radioactive Material Control (02.04)

a.

Inspection Scope

The inspectors observed locations where the licensee monitors potentially contaminated

material leaving the radiological control area and inspected the methods used for

control, survey, and release from these areas. The inspectors observed the

performance of personnel surveying and releasing material for unrestricted use and

evaluated whether the work was performed in accordance with plant procedures and

whether the procedures were sufficient to control the spread of contamination and

prevent unintended release of radioactive materials from the site. The inspectors

assessed whether the radiation monitoring instrumentation had appropriate sensitivity for

the type(s) of radiation present.

33

The inspectors reviewed the licensees criteria for the survey and release of potentially

contaminated material. The inspectors evaluated whether there was guidance on how to

respond to an alarm that indicates the presence of licensed radioactive material.

The inspectors reviewed the licensees procedures and records to verify that the

radiation detection instrumentation was used at its typical sensitivity level based on

appropriate counting parameters. The inspectors assessed whether or not the licensee

has established a de facto release limit by altering the instruments typical sensitivity

through such methods as raising the energy discriminator level or locating the instrument

in a high-radiation background area.

The inspectors selected several sealed sources from the licensees inventory records

and assessed whether the sources were accounted for and verified to be intact.

The inspectors evaluated whether any transactions, since the last inspection, involving

nationally tracked sources were reported in accordance with 10 CFR 20.2207.

b.

Findings

No findings were identified.

.4

Radiological Hazards Control and Work Coverage (02.05)

a.

Inspection Scope

The inspectors evaluated ambient radiological conditions (e.g., radiation levels or

potential radiation levels) during tours of the facility. The inspectors assessed whether

the conditions were consistent with applicable posted surveys, radiation work permits,

and worker briefings.

The inspectors evaluated the adequacy of radiological controls, such as required

surveys, radiation protection job coverage (including audio and visual surveillance for

remote job coverage), and contamination controls. The inspectors evaluated the

licensees use of electronic personal dosimeters in high noise areas as high radiation

area monitoring devices.

The inspectors reviewed the application of dosimetry to effectively monitor exposure to

personnel in high-radiation work areas with significant dose rate gradients.

The inspectors reviewed the following radiation work permits for work within airborne

radioactivity areas with the potential for individual worker internal exposures:

RWP 141100; U1C26 - Refuel Cavity Decontamination Activities;

RWP 141148; U1C26 - Steam Generator Platform Activities; and

RWP 141145; U1C26 - Valve Maintenance / Repair.

For these radiation work permits, the inspectors evaluated airborne radioactive controls

and monitoring, including potential for significant airborne levels (e.g., grinding, grit

blasting, system breaches, entry into tanks, cubicles, and reactor cavities). The

inspectors assessed barrier (e.g., tent or glove box) integrity and temporary

high-efficiency particulate air ventilation system operation.

34

The inspectors examined the licensees physical and programmatic controls for highly

activated or contaminated materials (i.e., nonfuel) stored within spent fuel and other

storage pools. The inspectors assessed whether appropriate controls (i.e.,

administrative and physical controls) were in place to preclude inadvertent removal of

these materials from the pool.

The inspectors examined the posting and physical controls for selected high radiation

areas and very-high radiation areas to verify conformance with the occupational

performance indicator.

b.

Findings

Failure to Identify Deficient Locked High Radiation Area Controls Due to Procedure

Inadequacy

Introduction: An NRC identified Green NCV of TS 5.4.1, Procedures, was identified for

inadequate procedures used to verify Locked High Radiation Controls in the Unit 2

Containment.

Description: On July 24, 2014, the inspector walked down the Unit 2 containment cavity

access ladder. At the time of the walkdown, the access to the cavity was posted LHRA

and had a ladder cage that functioned as a ladder lock device, in addition to a four-foot

high locked gate for access to the permanently installed cavity ladder. Discussions with

Radiation Protection staff had identified that the ladder lock device was not in place in

March 2014. Additionally, it was established that the locking cage was not placed back

on the ladder following the refueling outage in October 2013 when the area was

conservatively posted as a LHRA as the dose rates in the containment cavity were not in

excess of 1000 millirem per hour at 30 centimeters. The inspector reviewed Survey

Number CNP-1311-0001, dated November 1, 2013, which was a survey of the Final

Containment Cavity Survey following the last refueling outage. This survey confirmed

that the highest dose in the accessible areas of the cavity were nominally 2400 millirem

per hour on contact, and 500 millirem per hour at 30 centimeters from the source with

the highest readings in the cavity lift system pit area following the cavity

decontamination. These dose rates would not constitute a LHRA (greater than

1000 millirem per hour at 30 centimeters.) The survey showed that the gate to the cavity

ladder was posted as a LHRA.

Licensee Procedure PMP-6010-RPP-003, High, Locked High, and VHRA Access,

Section 3.3.5, directs weekly LHRA and VHRA verifications. Additional procedure

guidance is provided in THG-026, Locked High Radiation Area, and Very-High Radiation

Weekly Verification Process, Data Sheet 1, LHRA/VHRA Status Sheet, with additional

management expectations and a tracking tool for door/gate verifications while used as a

field guide for verifying LHRA/VHRA controls (i.e., doors/gates). The inspector identified

a substantial procedural weakness in this guidance in that the Data Sheet apparently did

not provide enough detail to direct Radiation Protection Technicians (RPTs) to verify that

the locked cage/ladder lock to the reactor cavity was in place and locked; a condition

which is necessary to provide reasonable assurance that the area is secured against

unauthorized access and cannot be easily circumvented. A review of the data verified

that RP staff did not identify the missing cage/ladder lock to the Unit 2 Reactor Cavity

ladder during weekly LHRA verification from November 2013 through March 2014. The

NRC inspectors also reviewed the LHRA and VHRA verification documentation in the

35

RP station daily logs from November 2013 to March 2014 and the inspectors did not

identify any discrepancies noted in the logs associated with in LHRA controls during their

weekly walkdowns of LHRA and VHRA verification. A review of the Corrective Action

Program documents did not identify a record of the missing ladder lock device or

identification of an unlocked LHRA. Therefore the licensee was not aware of the

deficient LHRA controls at the Unit 2 cavity ladder until it was discussed with the

inspectors. The failure to identify deficient LHRA controls could have the potential failure

to identify and report a Performance Indicator (PI) occurrence.

Analysis: The inspectors determined that there was an inadequacy in the licensees

procedure for identifying a deficient Locked High Radiation Area for the barrier in their

weekly locked cage/ladder barrier to the cavity of Unit 2 containment. The inspectors

determined that the procedure did not provide clear directions to assure the Radiation

Protection Technician would verify the required controls for LHRA is a performance

deficiency. The inspectors determined that the cause of the performance deficiency was

reasonably within the licensees ability to foresee and correct and should have been

prevented.

The finding was not subject to traditional enforcement since the incident did not have a

significant safety consequence, did not impact the NRCs ability to perform its regulatory

function, and was not willful.

The inspectors determined that the performance deficiency was more than minor in

accordance with IMC 0612, Appendix B, Issue Screening, because if left uncorrected,

the performance deficiency could lead to a more significant safety concern. Specifically,

the failure to identify deficient LHRA controls could result in unintentional exposure to

high levels of radiation.

The finding was assessed using the Occupational Radiation Safety SDP and was

determined to be of very-low safety significance because the problem was not an

ALARA planning issue, there were no overexposures nor substantial potential for

overexposures given the highest dose rates present in the room, the scope of work, and

the licensees ability to assess dose was not compromised.

The inspectors did not identify a corresponding cross-cutting aspect for this performance

deficiency.

Enforcement: Technical Specification 5.4.1, Procedures, requires that written

procedures shall be established, implemented and maintained covering the activities

referenced in Appendix A of Regulatory Guide 1.33, Revision 2. Control of Radioactivity

procedures, including limiting personnel exposure, are specified in Appendix A.

Contrary to the above, Procedure PMP-6010-RPP-003, High, Locked High, and

Very-High Radiation Area Access, Section 3.3.5, LHRA and VHRA Door/Gate

verification in conjunction with Procedural Guidance THG-026, Locked High Radiation

Area, and Very-High Radiation Weekly Verification Process did not provide sufficient

details to direct RPTs to verify that the locked cage/ladder lock to the reactor cavity was

in place and locked; a condition which is necessary to provide reasonable assurance

that the area is secured against unauthorized access and cannot be easily

circumvented. Consequently, weekly, from November 1, 2013, to March 2014 multiple

36

RPTs verified the Unit 2 Upper Containment Cavity gate was locked, but did not secure

the area against unauthorized access.

Corrective actions included review and revision of Procedure PMP-6010-RPP-003, High,

Locked High, and Very-High Radiation Area Access, and the associated Procedural

Guidance THG-026, Locked High Radiation Area and Very-High Radiation Weekly

Verification. Because this violation is of very-low safety significance and it was entered

into the licensees CAP as AR 2014-9001, this violation is being treated as an NCV

consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000315/2014005-06; 05000316/2014005-06; Failure to Identify Deficient

Locked High Radiation Area Controls Due to Procedure Inadequacy)

.5

Risk Significant High Radiation Area and Very-High Radiation Area Controls (02.06)

a.

Inspection Scope

The inspectors discussed with the radiation protection manager the controls and

procedures for high-risk, high radiation areas and very-high radiation areas. The

inspectors discussed methods employed by the licensee to provide stricter control of

very-high radiation area access as specified in 10 CFR 20.1602, Control of Access to

Very-High Radiation Areas, and Regulatory Guide 8.38, Control of Access to High and

Very-High Radiation Areas of Nuclear Plants. The inspectors assessed whether any

changes to licensee procedures substantially reduce the effectiveness and level of

worker protection.

The inspectors discussed the controls in place for special areas that have the potential

to become very-high radiation areas during certain plant operations with first-line health

physics supervisors (or equivalent positions having backshift health physics oversight

authority). The inspectors assessed whether these plant operations require

communication beforehand with the health physics group, so as to allow corresponding

timely actions to properly post, control, and monitor the radiation hazards including

re-access authorization.

The inspectors evaluated licensee controls for very-high radiation areas and areas with

the potential to become a very-high radiation areas to ensure that an individual was not

able to gain unauthorized access to the very-high radiation areas.

b.

Findings

No findings were identified.

.6

Radiation Worker Performance (02.07)

a.

Inspection Scope

The inspectors observed radiation worker performance with respect to stated radiation

protection work requirements. The inspectors assessed whether workers were aware of

the radiological conditions in their workplace and the radiation work permit controls/limits

in place, and whether their performance reflected the level of radiological hazards

present.

37

b.

Findings

No findings were identified.

.7

Radiation Protection Technician Proficiency (02.08)

a.

Inspection Scope

The inspectors observed the performance of the radiation protection technicians with

respect to all radiation protection work requirements. The inspectors evaluated whether

technicians were aware of the radiological conditions in their workplace and the radiation

work permit controls/limits, and whether their performance was consistent with their

training and qualifications with respect to the radiological hazards and work activities.

b.

Findings

No findings were identified.

.8

Problem Identification and Resolution (02.09)

a.

Inspection Scope

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensees Corrective Action Program. The

inspectors assessed the appropriateness of the corrective actions for a selected sample

of problems documented by the licensee that involve radiation monitoring and exposure

controls. The inspectors assessed the licensees process for applying operating

experience to their plant.

b.

Findings

No findings were identified.

2RS2 Occupational As-Low-As-Reasonably-Achievable Planning and Controls (71124.02)

The inspection activities supplement those documented in NRC Inspection Report

05000315-05000316/2014002 and constitute a partial sample as defined in Inspection

Procedure 71124.02-05.

.1

Radiation Worker Performance (02.05)

a.

Inspection Scope

The inspectors observed radiation worker and radiation protection technician

performance during work activities being performed in radiation areas, airborne

radioactivity areas, or high radiation areas. The inspectors evaluated whether workers

demonstrated the ALARA philosophy in practice (e.g., workers are familiar with the work

activity scope and tools to be used, workers used ALARA low-dose waiting areas) and

whether there were any procedure compliance issues (e.g., workers are not complying

with work activity controls). The inspectors observed radiation worker performance to

assess whether the training and skill level was sufficient with respect to the radiological

hazards and the work involved.

38

b.

Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program (71124.07)

This inspection constituted one complete sample as defined in Inspection Procedure

71124.07-05.

.1

Inspection Planning (02.01)

a.

Inspection Scope

The inspectors reviewed the annual radiological environmental operating reports and the

results of any licensee assessments since the last inspection to assess whether the

Radiological Environmental Monitoring Program was implemented in accordance with

the Technical Specifications and Offsite Dose Calculation Manual. This review included

reported changes to the Offsite Dose Calculation Manual with respect to environmental

monitoring, commitments in terms of sampling locations, monitoring and measurement

frequencies, land use census, Inter-Laboratory Comparison Program, and analysis of

data.

The inspectors reviewed the Offsite Dose Calculation Manual to identify locations of

environmental monitoring stations.

The inspectors reviewed the Final Safety Analysis Report for information regarding the

environmental monitoring program and meteorological monitoring instrumentation.

The inspectors reviewed quality assurance audit results of the program to assist in

choosing inspection smart samples. The inspectors also reviewed audits and technical

evaluations performed on the vendor laboratory if used.

The inspectors reviewed the annual effluent release report and the 10 CFR Part 61,

Licensing Requirements for Land Disposal of Radioactive Waste, report, to determine if

the licensee was sampling, as appropriate, for the predominant and dose-causing

radionuclides likely to be released in effluents.

b.

Findings

No findings were identified.

.2

Site Inspection (02.02)

a.

Inspection Scope

The inspectors walked down select air sampling stations and dosimeter monitoring

stations to determine whether they were located as described in the Offsite Dose

Calculation Manual and to determine the equipment material condition. Consistent with

smart sampling, the air sampling stations were selected based on the locations with the

highest X/Q, D/Q wind sectors, and dosimeters were selected based on the most risk

significant locations (e.g., those that have the highest potential for public dose impact).

39

For the air samplers and dosimeters selected, the inspectors reviewed the calibration

and maintenance records to evaluate whether they demonstrated adequate operability of

these components. Additionally, the review included the calibration and maintenance

records of select composite water samplers.

The inspectors assessed whether the licensee had initiated sampling of other

appropriate media upon loss of a required sampling station.

The inspectors observed the collection and preparation of environmental samples from

different environmental media (e.g., ground and surface water, milk, vegetation,

sediment, and soil) as available to determine whether environmental sampling was

representative of the release pathways as specified in the Offsite Dose Calculation

Manual and if sampling techniques were in accordance with procedures.

Based on direct observation and review of records, the inspectors assessed whether

the meteorological instruments were operable, calibrated, and maintained in

accordance with guidance contained in the Final Safety Analysis Report, NRC

Regulatory Guide 1.23, Meteorological Monitoring Programs for Nuclear Power Plants,

and licensee procedures. The inspectors assessed whether the meteorological data

readout and recording instruments in the control room and, if applicable, at the tower

were operable.

The inspectors evaluated whether missed and/or anomalous environmental samples

were identified and reported in the annual environmental monitoring report. The

inspectors selected events that involved a missed sample, inoperable sampler, lost

dosimeter, or anomalous measurement to determine if the licensee had identified the

cause and had implemented corrective actions. The inspectors reviewed the licensees

assessment of any positive sample results (i.e., licensed radioactive material detected

above the lower limits of detection) and reviewed the associated radioactive effluent

release data that was the source of the released material.

The inspectors selected structures, systems, or components that involve or could

reasonably involve licensed material for which there is a credible mechanism for

licensed material to reach ground water, and assessed whether the licensee had

implemented a sampling and monitoring program sufficient to detect leakage of these

structures, systems, or components to ground water.

The inspectors evaluated whether records, as required by 10 CFR 50.75(g), of leaks,

spills, and remediation since the previous inspection were retained in a retrievable

manner.

The inspectors reviewed any significant changes made by the licensee to the Offsite

Dose Calculation Manual as the result of changes to the land census, long-term

meteorological conditions (3-year average), or modifications to the sampler stations

since the last inspection. They reviewed technical justifications for any changed

sampling locations to evaluate whether the licensee performed the reviews required to

ensure that the changes did not affect its ability to monitor the impacts of radioactive

effluent releases on the environment.

The inspectors assessed whether the appropriate detection sensitivities with respect to

Technical Specifications/Offsite Dose Calculation Manual where used for counting

40

samples (i.e., the samples meet the technical specifications/Offsite Dose Calculation

Manual required lower limits of detection). The inspectors reviewed quality control

charts for maintaining radiation measurement instrument status and actions taken for

degrading detector performance. The licensee uses a vendor laboratory to analyze the

radiological environmental monitoring program samples so the inspectors reviewed the

results of the vendors quality control program, including the inter-laboratory comparison,

to assess the adequacy of the vendors program.

The inspectors reviewed the results of the licensees Inter-Laboratory Comparison

Program to evaluate the adequacy of environmental sample analyses performed by the

licensee. The inspectors assessed whether the inter-laboratory comparison test

included the media/nuclide mix appropriate for the facility. If applicable, the inspectors

reviewed the licensees determination of any bias to the data and the overall effect on

the radiological environmental monitoring program.

b.

Findings

No findings were identified.

.3

Identification and Resolution of Problems (02.03)

a.

Inspection Scope

The inspectors assessed whether problems associated with the radiological

environmental monitoring program were being identified by the licensee at an

appropriate threshold and were properly addressed for resolution in the licensees

Corrective Action Program. Additionally, they assessed the appropriateness of the

corrective actions for a selected sample of problems documented by the licensee that

involved the radiological environmental monitoring program.

b.

Findings

No findings were identified.

4.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, and Occupational and Public Radiation Safety

4OA1 Performance Indicator Verification (71151)

.1

Mitigating Systems Performance Index - Emergency AC Power System

a.

Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index (MSPI) - Emergency AC Power System performance

indicator for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013

through the second quarter 2014. To determine the accuracy of the PI data reported

during those periods, PI definitions and guidance contained in the Nuclear Energy

Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 7, dated August 31, 2013, were used. The inspectors reviewed the

41

licensees operator narrative logs, MSPI derivation reports, issue reports, event reports

and NRC Integrated Inspection Reports for the period of July 2013 through June 2014 to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

NEI guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report. Portions of this inspection activity were credited in NRC

Inspection Report 05000315-05000316/2014004.

This inspection constituted one MSPI emergency AC power system sample as defined in

IP 71151-05.

b.

Findings

No findings were identified.

.2

Mitigating Systems Performance Index - High Pressure Injection Systems

a.

Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - High Pressure Injection Systems performance indicator

for Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter of 2013 thru

the third quarter of 2014. To determine the accuracy of the PI data reported during

those periods, PI definitions and guidance contained in the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August 31,

2013, were used. The inspectors reviewed the licensees operator narrative logs, issue

reports, MSPI derivation reports, event reports and NRC Integrated Inspection Reports

for the period of the third quarter of 2013 thru the 2nd quarter of 2014 to validate the

accuracy of the submittals. The inspectors reviewed the MSPI component risk

coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

NEI guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report. Portions of this inspection activity were credited in NRC

Inspection Report 05000315-05000316/2014004.

This inspection constituted one MSPI high pressure injection system sample as defined

in IP 71151-05.

b.

Findings

No findings were identified.

42

.3

Mitigating Systems Performance Index - Heat Removal System

a.

Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - Heat Removal System performance indicator for

Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the

second quarter 2014. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

event reports, MSPI derivation reports, and NRC Integrated Inspection Reports for the

period of July 2013 through June 2014 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report. Portions of this

inspection activity were credited in NRC Inspection Report

05000315-05000316/2014004.

This inspection constituted one MSPI heat removal system sample as defined in

IP 71151-05.

b.

Findings

No findings were identified.

.4

Mitigating Systems Performance Index - Residual Heat Removal System

a.

Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - Residual Heat Removal System performance indicator for

Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the

second quarter 2014. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the

period of July 2013 through June 2014 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report. Portions of this

inspection activity were credited in NRC Inspection Report

05000315-05000316/2014004.

43

This inspection constituted one MSPI residual heat removal system sample as defined in

IP 71151-05.

b.

Findings

No findings were identified.

.5

Mitigating Systems Performance Index - Cooling Water Systems

a.

Inspection Scope

In the third quarter of 2014, the inspectors sampled licensee submittals for the Mitigating

Systems Performance Index - Cooling Water Systems performance indicator for

Donald C. Cook Unit 1 and Unit 2 for the period from the third quarter 2013 through the

second quarter 2014. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

MSPI derivation reports, event reports and NRC Integrated Inspection Reports for the

period of July 2013 through June 2014 to validate the accuracy of the submittals. The

inspectors reviewed the MSPI component risk coefficient to determine if it had changed

by more than 25 percent in value since the previous inspection, and if so, that the

change was in accordance with applicable NEI guidance. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report. Portions of this

inspection activity were credited in NRC Inspection Report

05000315-05000316/2014004.

This inspection constituted one MSPI cooling water system sample as defined in

IP 71151-05.

b.

Findings

No findings were identified.

.6

Reactor Coolant System Leakage

a.

Inspection Scope

The inspectors sampled licensee submittals for the RCS Leakage performance indicator

for both Unit 1 and 2 for the period from the fourth quarter 2013 through the third quarter

2014. To determine the accuracy of the PI data reported during those periods, PI

definitions and guidance contained in the NEI Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 31, 2013, were

used. The inspectors reviewed the licensees operator logs, RCS leakage tracking data,

issue reports, event reports and NRC Integrated Inspection Reports for the period of the

fourth quarter 2013 through the third quarter 2014 to validate the accuracy of the

submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator and none were identified. Documents reviewed are listed in the

Attachment to this report.

44

This inspection constituted two RCS leakage samples as defined in IP 71151-05.

b.

Findings

No findings were identified.

.7

Reactor Coolant System Specific Activity

a.

Inspection Scope

The inspectors sampled licensee submittals for the RCS specific activity Performance

Indicator for D.C. Cook Nuclear Power Plant Units 1 and 2 for the period from the third

quarter 2013 through the third quarter 2014. The inspectors used Performance Indicator

definitions and guidance contained in the Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 7, dated August

2013, to determine the accuracy of the Performance Indicator data reported during those

periods. The inspectors reviewed the licensees RCS chemistry samples, Technical

Specification requirements, issue reports, event reports, and NRC Integrated Inspection

Reports to validate the accuracy of the submittals. The inspectors also reviewed the

licensees issue report database to determine if any problems had been identified with

the Performance Indicator data collected or transmitted for this indicator and none were

identified. In addition to record reviews, the inspectors observed a chemistry technician

obtain and analyze a RCS sample. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted two RCS specific activity samples as defined in IP 71151-05.

b.

Findings

No findings were identified.

.8

Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a.

Inspection Scope

The inspectors sampled licensee submittals for the radiological effluent Technical

Specification/Offsite Dose Calculation Manual radiological effluent occurrences

Performance Indicator for the period from the third quarter 2013 through the third quarter

2014. The inspectors used Performance Indicator definitions and guidance contained in

the Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 7, dated August 2013, to determine the accuracy of the

Performance Indicator data reported during those periods. The inspectors reviewed the

licensees issue report database and selected individual reports generated since this

indicator was last reviewed to identify any potential occurrences such as unmonitored,

uncontrolled, or improperly calculated effluent releases that may have impacted offsite

dose. The inspectors reviewed gaseous effluent summary data and the results of

associated offsite dose calculations for selected dates to determine if indicator results

were accurately reported. The inspectors also reviewed the licensees methods for

quantifying gaseous and liquid effluents and determining effluent dose. Documents

reviewed are listed in the Attachment to this report.

45

This inspection constituted one Radiological Effluent Technical Specification/Offsite

Dose Calculation Manual radiological effluent occurrences sample as defined in

IP 71151 05.

b.

Findings

No findings were identified.

.9

Occupational Exposure Control Effectiveness

a.

Inspection Scope

The inspectors sampled licensee submittals for the Occupational Exposure Control

Effectiveness Performance Indicator for the period from the third quarter 2013 through

the third quarter 2014. The inspectors used Performance Indicator definitions and

guidance contained in the Nuclear Energy Institute Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 7, dated August 2013, to

determine the accuracy of the Performance Indicator data reported during those periods.

The inspectors reviewed the licensees assessment of the Performance Indicator for

occupational radiation safety to determine if the indicator related data was adequately

assessed and reported. To assess the adequacy of the licensees Performance

Indicator data collection and analyses, the inspectors discussed with radiation protection

staff the scope and breadth of its data review and the results of those reviews. The

inspectors independently reviewed electronic personal dosimetry dose rate and

accumulated dose alarms and dose reports and the dose assignments for any intakes

that occurred during the time period reviewed to determine if there were potentially

unrecognized occurrences. The inspectors also conducted walkdowns of numerous

locked high and very-high radiation area entrances to determine the adequacy of the

controls in place for these areas. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted one occupational exposure control effectiveness sample as

defined in IP 71151-05.

b.

Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1

Routine Review of Items Entered into the Corrective Action Program

a.

Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify they were being entered into the licensees CAP at an

appropriate threshold, that adequate attention was being given to timely corrective

46

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

Findings

No findings were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for followup, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b.

Findings

No findings were identified.

.3

Semiannual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the 6-month period of July 2014 through December 2014,

although some examples expanded beyond those dates where the scope of the trend

warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

47

reports, self-assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees CAP

trending reports. Corrective actions associated with a sample of the issues identified in

the licensees trending reports were reviewed for adequacy.

The inspectors observed some weaknesses in different aspects of the operability

determination process. There were some instances where ARs were written but were

not flagged for an operability review. Some had been already identified by the licensee

upon questioning by the inspectors, others had not. In these cases, the inspectors did

not find any instances where equipment should have been called inoperable but was

not. The inspectors also found a functionality assessment associated with fire pumps

where necessary compensatory measures were not formalized until the inspectors had

questioned the assessment. During the period of review, there were two NRC identified

findings with identified weaknesses in the operability determination process. One was

documented in NRC Inspection Report 2014004 and dealt with a failure to provide

adequate technical justification for operability of a TDAFW pump with respect to

governor oil levels. Another issue is documented in Section 1R15 of this report and

dealt with, in part, appropriate oil levels for TDAFW bearings. The inspectors discussed

the observations with licensee staff, who agreed with the assessment.

The inspectors also observed weaknesses in work planning and execution. Multiple

instances were identified of scheduled work activities that had to be de-conflicted the

day/week of execution. In some cases, procedures had to be revised to support work, or

post-maintenance test activities changed to appropriately cover the scope of work near

time of execution. In some cases, where changes were made or expanded scope

encountered, the plant risk summary sheet (a vehicle by which the plant risk is conveyed

to the site) was not updated appropriately. A finding in Section 1R15 of this report

documents a case where inadequate planning and execution unexpectedly rendered a

diesel fuel oil storage tank inoperable. Inspectors have discussed the issue with

licensee staff, who agreed with the assessment.

This review constituted one semiannual trend inspection sample as defined in

IP 71152-05.

b.

Findings

No findings were identified.

.4

Selected Issue Followup Inspection: Review of Operator Workarounds

a.

Inspection Scope

The inspectors evaluated the licensees implementation of their process used to identify,

document, track, and resolve operational challenges. Inspection activities included, but

were not limited to, a review of the cumulative effects of the operator workarounds

(OWAs) on system availability and the potential for improper operation of the system, for

potential impacts on multiple systems, and on the ability of operators to respond to plant

transients or accidents.

The inspectors performed a review of the cumulative effects of OWAs. The documents

listed in the Attachment to this report were reviewed to accomplish the objectives of the

inspection procedure. The inspectors reviewed both current and historical operational

48

challenge records to determine whether the licensee was identifying operator challenges

at an appropriate threshold, had entered them into their CAP and proposed or

implemented appropriate and timely corrective actions which addressed each issue.

Reviews were conducted to determine if any operator challenge could increase the

possibility of an Initiating Event, if the challenge was contrary to training, required a

change from long-standing operational practices, or created the potential for

inappropriate compensatory actions. Additionally, all temporary modifications were

reviewed to identify any potential effect on the functionality of Mitigating Systems,

impaired access to equipment, or required equipment uses for which the equipment was

not designed. Daily plant and equipment status logs, degraded instrument logs, and

operator aids or tools being used to compensate for material deficiencies were also

assessed to identify any potential sources of unidentified operator workarounds.

This review constituted one in depth review of a selected issue sample (operator work

arounds) as defined in IP 71152-05.

b.

Findings

No findings were identified.

.5

Selected Issue Follow-up Inspection: Follow-up to Previous NRC Findings

a.

Inspection Scope

The inspectors selected a sample of previously issued NRC findings to assess the

adequacy of licensee corrective actions. Two instances were identified where the

technical issues had been adequately addressed; however, it appeared there were no

corrective actions for underlying performance issues. In one case, a finding was issued

regarding a change in the system pressures at which the fire pumps would automatically

start (NCV 05000315-05000316/2013009-02). While the licensee was able to eventually

show the new setpoints were acceptable, nothing was done to explore potential

breakdowns in the engineering change process or in human performance that allowed

the change to occur without the additional reviews being done to begin with. In another

example, FIN 05000315-05000316/2013002-02 was issued for a failure to follow the

guidance in the operability determination procedure. Subsequently, the licensee used

methods that were acceptable to validate the past operability of Emergency Core

Cooling piping when a void was discovered. However, any underlying issues in human

performance or in the operability determination process were not explored at the time.

The licensee acknowledged the inspectors observations.

Regarding the finding discussed above for the fire pump starting setpoints, the

inspectors also identified that changes had been made to the plant design basis since

the licensees previous corrective actions were completed. Pursuant to the change to

NFPA-805 standards of fire protection, additional sprinklers were added to the required

Technical Requirements Manual fire suppression systems. When this occurred, the

licensee did not re-review the impacts on the fire pump starting setpoint issue which was

the subject of the NRC finding. Based on inspector questions, the licensee re-instituted

compensatory measures to restore functionality of the fire suppression system pending

approval of new calculations that will incorporate the new systems and starting setpoints

of the fire pumps. Additionally, the inspectors questioned the adequacy of current fire

pump surveillance tests in light of the NRC finding. The inspectors discovered the

49

licensee had already identified a discrepancy between the surveillance tests and design

requirements and had written an AR in September of 2014. Basically, a pump could

degrade to a point where it would still pass a surveillance, yet not meet all aspects of the

design calculation requirements for the fire suppression system. The licensee was able

to demonstrate the pumps had not degraded to a point outside the design requirements,

and was working to resolve the discrepancy between the tests and design requirements.

This review constituted one in-depth review of a selected issue sample as defined in

IP 71152-05.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1

Dual Unit Trip Caused by Debris Intrusion in the Forebay

a.

Inspection Scope

On November 1, 2014, the inspectors responded to the site following a dual unit trip

caused by debris intrusion in the forebay of the screenhouse. During the evening of

October 31, and early morning of November 1, rough lake conditions and high wind

mobilized and transported a large mass of sea grass and other debris. This debris

entered the D.C. Cook intake structure and collected on trash racks and travelling

screens in the fore bay. Prior to the unit shutdown, the licensee monitored forebay

conditions and took actions to maintain the travelling screens clean. However, the rate

of debris intrusion exceeded the equipments ability to clean the screens. As differential

pressure increased across the screens, the licensee entered the Degraded Forebay

abnormal procedure. The licensee reduced power in Unit 2 to 50 percent and secured a

circulating water pump. However, conditions in the fore bay continued to degrade to the

point that the licensee had to manually trip both units. This action allowed the licensee

to secure all circulating water pumps thus protecting the safety-related service water

system.

Following the plant trip, the licensee notified the resident inspector who responded to the

site. The inspectors verified licensee actions in the control rooms were consistent with

plant procedures. In addition, the inspectors focused on performance of safety-related

equipment supplied with service water. The inspectors concluded that the service water

system had not been impacted by the debris intrusion.

As part of the plant shutdown, several plant SSCs did not perform as expected. For

Unit 2, auto transfer between the unit auxiliary transformer and reserve auxiliary

transformer on turbine trip did not occur. Auto transfer did occur after the licensee

manually inserted a generator trip. The licensee replaced a failed relay associated with

a turbine stop valve to correct the condition. In addition, a relay on the unit two reserve

auxiliary transformer failed that precluded auto-stepping of the transformer; the licensee

replaced this relay prior to unit startup.

On Unit 1, the turbine driven auxiliary feedwater pump tripped while the licensee

throttled flow. Because both MDAFW pumps were operable, the licensee used the

MDAFW pumps for steam generator level control. The inspectors identified a finding as

documented in Section 1R15 of this report. Additionally, on Unit 2, an AFW flow control

valve appeared to not respond to a flow retention signal. The flow retention circuit acts

to prevent excessive flows to the steam generators from the AFW pumps by throttling

50

closed flow control valves. Upon investigation, given instrument tolerances, tests of the

circuitry, time delay settings, and actual measured flow, it was determined the system

acted appropriately.

In addition, three steam safety valves lifted prior to their nominal set point tolerance

band. In reviewing the condition, the licensee documented that set point surveillances

are conducted using a defined set of conditions that allow the safeties to achieve

repeatable lift setpoints. For an installed safety, several factors can influence actual lift

pressure. These factors include vibration and temperature transients. As a result, the

licensee concluded that the valves responded in a fashion consistent with the design of

the valves. The licensee plans on performing lift tests on the valves during the next

refueling outage to confirm valve operability.

This event follow-up review constituted one sample as defined in IP 71153-05.

b.

Findings

No findings were identified.

4OA6 Management Meetings

.1

Exit Meeting Summary

On January 20, 2015, the inspectors presented the inspection results to Mr. L. Weber

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed

was considered proprietary.

.2

Interim Exit Meetings

Interim exits were conducted for:

The results of the inservice inspection were discussed with site vice president,

Mr. J. Gebbie on October 10, 2014;

The inspection results for the areas of radiological hazard assessment and

exposure controls; occupational ALARA planning and controls; and occupational

exposure control effectiveness performance indicator verification with

Mr. J. Gebbie, Site Vice President, on October 17, 2014;

The inspection results for the area of radiological hazard assessment and

exposure controls with Mr. J. Gebbe, Site Vice President, on October 29, 2014;

The inspection results for the areas of radiological environmental monitoring; and

RCS specific activity and RETS/ODCM radiological effluent occurrences

performance indicator verification with Mr. J. Gebbe, Site Vice President, on

November 7, 2014;

The results of the inspection of the permanent removal of shield/missile blocks

with Mr. L. Weber, Chief Nuclear Officer, and other members of the licensee staff

on December 01, 2014; and

The Annual Review of Emergency Action Level and Emergency Plan Changes

with the Licensee's Chief Nuclear Officer, Mr. L. Weber, on January 12, 2015.

51

The inspectors confirmed that none of the potential report input discussed was

considered proprietary. Proprietary material received during the inspection was returned

to the licensee.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

L. Weber, Chief Nuclear Officer

J. Gebbie, Site Vice President

L. Baun, Director Performance Assurance

J. Beer, Principal Health Physicist

D. Bronicki, Interim Radiation Protection Manager

R. Hall, ISI Program Owner

J. Harner, Environmental Manager

G. Hill, Supervisor Nuclear Safety Analysis

S. Lies, Vice President Engineering

S. Mitchell, Regulatory Affairs

D. Miller, Health Physicist

J. Nimtz, Senior Licensing Activity Coordinator

J. Ross, Engineering Director

M. Scarpello, Regulatory Affairs Manager

P. Schoepf, Nuclear Site Services Director

R. Sieber, Emergency Preparedness Manager

Nuclear Regulatory Commission

K. Riemer, Chief, Reactor Projects Branch 2

R. Daley, Chief, Engineering Branch 3

B. Dickson, Chief, Health Physics and Incident Response

N. Feliz-Adorno, Reactor Engineer

J. Gilliam; Reactor Engineer

M. Mitchell, Health Physicist

2

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened 05000315/2014005-01

NCV

Failure to Identify Conditions Adverse to Quality

associated with the Unit 1 TDAFW Pump Turbine Oil

System (Section 1R15.b(1))05000315/2014005-02; 05000316/2014005-02

NCV

Unplanned Inoperability of the AB Fuel Oil Storage Tank

during Maintenance (Section 1R15.b(2))05000315/2014005-03; 05000316/2014005-03

NCV

Inadequate Review of Radiological Impact of the Removal

of the Auxiliary Shield Blocks on the Containment

Accident Shield Post LBLOCA (Section 1R18)05000315/2014005-04

NCV

Inadvertent Trip of the Unit 1 TDAFW Pump

(Section 1R19)05000315/2014005-05

URI

Changes to Minimum 60-Minute Emergency Responder

Staffing Without Prior Approval (Section 1EP4)05000315/2014005-06; 05000316/2014005-06

NCV

Failure To Identify Deficient Locked High Radiation Area

Controls Due To Procedure Inadequacy (Section 2RS1.4)

Closed 05000315/2014005-01

NCV

Failure to Identify Conditions Adverse to Quality

associated with the Unit 1 TDAFW Pump Turbine Oil

System (Section 1R15.b(1))05000315/2014005-02; 05000316/2014005-02

NCV

Unplanned Inoperability of the AB Fuel Oil Storage Tank

during Maintenance (Section 1R15.b(2))05000315/2014005-03; 05000316/2014005-03

NCV

Inadequate Review of Radiological Impact of the Removal

of the Auxiliary Shield Blocks on the Containment

Accident Shield Post LBLOCA (Section 1R18)05000315/2014005-04

NCV

Inadvertent Trip of the Unit 1 TDAFW Pump

(Section 1R19)05000315/2014005-06; 05000316/2014005-06

NCV

Failure To Identify Deficient Locked High Radiation Area

Controls Due To Procedure Inadequacy (Section 2RS1.4)

Discussed

None

3

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

- 12-IHP-5040-EMP-004, Plant Winterization and De-Winterization, Revision 21

- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7

- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22

- AR-2014-14403, 12-HV-DGH Appears to Have Failed

- Cook Seasonal Readiness Affirmation Letter, November 11, 2014

- PMP-5055-001-001, Winterization/Summerization Checklist, Revision 22

1R04 Equipment Alignment

- 2-OHP-4021-017-002, Placing in Service the Residual Heat Removal System, Revision 24

- 2-OHP-4030-217-050W, West Residual Heat Removal Train Operability Test, Modes 1-4,

Revision 14

- AR-2014-14089, CTS Nozzle Leaking

- AR-2014-8502, Possible PORV Leakby

- Drawing OP-1-5144-51, Containment Spray

- Drawing OP-2-5105D-22, Steam Generating System

- Drawing OP-2-5106A-55, Aux Feedwater

- List of Open Work Orders, Unit 1 Containment Spray System

1R05 Fire Protection

- AR 2014-15683, Combustible Material Stored in 2AB DB FO Transfer Pump Room

- AR-2014-12540, Unattended Test Equipment

- CNP Fire Safety Analysis, Report R1900-007-AA32, Fire Area 32, June 2011

- Fire Hazards Analysis, Revision 16

- PMP-2270-CCM-001, Control of Combustible Materials, Revision 24

- PMP-2270-WBG-001, Welding, Burning, and Grinding Activities, Revision 23

1R06 Flooding

- 12-1141-53, 34.5Kv & 4 Kv Power Duct Runs & Control Cable Pipe Runs in Plant Yard Area,

April 4, 1971

1R07 Heat Sink Performance

- 12-EHP-8913-001-002, Heat Exchanger Inspection, Revision 9

- D.C. Cook Commitment Change Number CC-0218, Regarding Heat Exchanger Inspection

Program, March 10, 2003

- Fall 2014 U1C26 Eddy Current Inspection Results, 1-HE-47-CDN Heat Exchanger

- NRC Generic Letter 89-13, Service Water System Problems Affecting Safety-Related

Equipment, July 18, 1989

4

1R08 Inservice Inspection Activities

- 12-EHP-5037-SGP-004, Steam Generator Foreign Object Disposition, Revision 5

- 12-EHP-5070-NDE-DMW, Ultrasonic Examination of ASME Section XI, Appendix VIII,

Supplement 10 Dissimilar Metal Welds, Revision 0

- 12-QHP-5050-NDE-002, Magnetic Particle Examination, Revision 6

- 12-QHP-5050-NDE-010, Radiographic Examination of Welds, Revision 6

- 1-EHP-4030-102-001, Steam Generator Primary Side Surveillance, Revision 10

- AR 2012-12105, Water Pooling Around U2 CST

- AR 2013-0534, 12-CS-185 has a Body to Bonnet Leak

- AR 2013-4317, 1-QRV-114, Body to Bonnet Leak

- AR 2013-4625, 1-CS-448-1 has a BA Leak

- AR 2013-5096, No. 14 SG Cold Leg Nozzle Dam Leakage

- AR 2013-5279, 12-QLA-420-IDH BA Leak from Swedgelock Fitting

- AR 2013-6540, 1-SF-160 Leaking at Diaphragm

- AR 2013-6839, U1C25 Refueling Cavity Leakage

- AR 2013-7061, 1-RH-147W has Boric Acic on Body to Bonnet

- AR 2013-7067, 1-RH-107W Leaks by at 0.095 ml/min

- AR 2013-7220, Reactor Head and Pressurizer Vent Piping Areas

- AR 2013-7354, Evidence of Previous Small Boric Acid Leak from 1-NFP-211

- AR 2013-7355, 1-NFP-240 has Evidence of Prior Test Fitting Leakage

- AR 2013-8587, U1 Seal Table Thimble Leakage Identified

- AR 2013-9459, 12-CS-185 has a Ruptured Diaphragm

- AR 2014-8869, 1-QRV-200, Active Boric Acid Leak on Packing

- AR 2014-11337, Wall Loss Identified in NESW Containment Penetration Piping

- AR 2014-11339, Piping Wall Loss Near 1-WCR-942

- AR 2014-11413, Six Data Points In Piping Found Below Manufact Tolerance

- AR 2014-11518, Six Data Points In Piping Found Below Design Minimum

- AR 2014-11519, Two Data Points In Piping Found Below Design Minimum

- AR 2014-11664, NESW Pipe Wall Below Manufacturers Tolerance

- AR 2014-12108, NRC Observation: Boric Acid not Included in GE I-8000

- AR 2014-12160, Technician Understanding of Range of Coverage Questioned

- AR 2014-12162, NRC Inservice Inspection Observation

- AR 2014-1218, AR for Boric Acid Leak Not Properly Screened

- AR 2014-12384, NRC Observation During U1 Inservice Inspection

- AR 2014-3762, Previously Identified BA Leak on 1-SI-128

- DIT-B-03569-01, AEP Design Information Transmittal, October 7, 2014

- ETSS No. 1, Bobbin Coil, Revision 0

- ETSS No. 2, 3 Coil MRPC, Revision 0

- LMT-04-UT-012, Manual Phased Array Ultrasonic Examination of Weld Overlaid Similar and

Dissimilar Metal Welds, Revision 0

- LMT-04-UT-113, Ultrasonic Examination of Nozzle Inner Radius Areas, Revision 7

- LMT-10-PAUT-002, Manual Phased Array Ultrasonic Examination of Austenitic and Ferritic

Piping Welds, Revision 0

- PDI-UT-11, Generic Procedure for the Ultrasonic Detection and Sizing of Reactor Pressure

Vessel Nozzle-to-Shell Welds and Nozzle Inner Radius, Revision C

- PMI-5070, Inservice Inspection, Revision 21

- PMP-5030-001-001, Boric Acid Corrosion Control, Revision 17

- PQR 136, ASME Procedure Qualification Record, Revision 1

- PQR 219, ASME Procedure Qualification Record, Revision 1

- PQR 256, ASME Procedure Qualification Record, Revision 1

5

- PQR 258, ASME Procedure Qualification Record, Revision 1

- QA-46, Qualification and Certification NDE and Visual Examination Personnel, Revision 3

- S000126-AST-000001, Steam Generator Degradation Assessment, Revision 0

- S000126-WKI-000020, D.C. Cook Unit 1 Steam Generator Eddy Current Testing Site

Technique Validation, Revision 0

- U1-MT-14-001, Magnetic Particle Examination, October 4, 2014

- U1-PT-14-004, Liquid Penetrant Examination, October 2, 2014

- U1-PT-14-005, Liquid Penetrant Examination, October 2, 2014

- U1-VE-14-003, Ultrasonic Examination, October 2, 2014

- U1-VE-14-004, Ultrasonic Examination, October 2, 2014

- U1-VE-14-014, Ultrasonic Examination, October 8, 2014

- UT-110, Ultrasonic Examination of Vessel Welds and Adjacent Base Metal >2.0 in Thickness,

Revision 2

- WO 55390312-01, Replacement of 1-NLI-112-V1, October 7, 2014

- WO 55392571-01, Replacement of 1-NRV-102, March 12, 2013

- WO 55404504-06, EC 52036, Install New Snubber Pipe Support 1-ARC-S-4012,

March 8, 2013

- WO 55421212-10/13, Replacement of 1-NFP-222-V2, March 6, 2013

- WO 55440759-05, Install Valve Assembly 1-CS-314, October 7, 2014z

- WPS 8.12T, Welding Procedure Specification, Revision 1

- WPS 8.1TS, Welding Procedure Specification, Revision 4

1R11 Licensed Operator Requilification Program

- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25

- November 19, 2014, Training Exercise Guide and Drill Guide

- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4

1R12 Maintenance Effectiveness

- 1-IHP-6030-IMP-002, NARPI System Operational Test and Linearization, Revision 11

- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11

- 2012-2013 AMSAC, Unavailability Hours Reports

- AR 2010-10345, U2 Letdown Isolation after Shutdown Due to RCS Cooldown

- AR 2012-14344, 2-URV-125 Failed To Stroke Fully Open

- AR 2012-14364-1, 1-NRI-16 Found Out of Spec

- AR 2012-16048, 1-URV-125 Failed Drop Test

- AR 2012-4275, Steam Dump System Operation

- AR 2013-10252, 1-URV-136 Failed Drop Test

- AR 2013-1157, 1-NRI-50 Lower Section Power Supply Out of Tolerance

- AR 2013-1164, 2-MRV-212 Failed Stroke Time

- AR 2013-11973, Unit 2 MS-02 has Exceeded its Unavailability Limit

- AR 2013-3420, Flux Differential Indicators Found Out of Tolerance

- AR 2013-4315, 1-MRV-231 Fail to Close Upon Return to Neutral

- AR 2013-4320, 1-URV-110 Failing to Open

- AR 2013-4349, 1-URV-112 Failed to Open When Required

- AR 2013-4373-1, U-1 Scaler/Timer did Not Have Audible Counts Following S/D

- AR 2013-5060, 1-URV-111 Would not Stroke During Testing

- AR 2013-6243, 2-MRV-212 Failed IST Stroke Times

- AR 2013-8216, 2-NRI-44B +25V Power Supply Degraded

- AR 2014-0045, 2-URV-120 Failed Drop Test

6

- AR 2014-11324, Steam Dumps Did Not Operate Per Procedure

- AR 2014-11739, Critical Parameter Found Out of Tolerance

- AR 2014-12621, 1-URV-112 Drop Test Failed

- AR 2014-13085, 1-URV-112 Has Been Failed for a Complete Cycle

- AR 2014-13088, Failure to Perform MRE on 1-URV-112 in U1C25

- AR 2014-13277, Unit 1 Main Steam Function MS-09 (a)(1) Process

- AR 2014-14971, Unit 2 Main Steam Function MS-05 (a)(1) Process

- AR 2014-15004, As Found Data Out of Tolerance

- AR 2014-15113, ACE and MRE in AR 2013-6243 Are Not In Agreement

- AR 2014-2686, 1-MRV-232 Exceeded Max Stroke Time Limit During PMT

- AR 2014-2719, 1-MRV-232 SG #3 Stop Valve Dump Valve

- AR-2013-10084, B6 Rod IRPI Lost During Maintenance, July 13, 2013

- AR-2013-12121, RPI Failure Rod D8, August 19, 2013

- AR-2013-19212, Unit 1 RPI for B6 Inoperable, December 17, 2013

- AR-2013-7039, 1-RPIS-M8-SC New Module Faulty, May 10, 2013

- AR-2013-7366, During Test Rod C7 Stayed at 0, May 17, 2013

- AR-2013-768, Control Bank D F-14 Rod Outside and, May 25, 2013

- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,

October 23, 2014

- ATWS Mitigation Actuation System (AMSAC) Maintenance Rule Scoping Document,

Revision 1

- GT 2013-11467, U2 MS Maintenance Rule Action Tracking

- GT 2013-11615, 2013 Main Steam System Vulnerability Review

- Maintenance Rule Scoping Document, AMSAC System, Revision 1

- Maintenance Rule Scoping Document, Control Rod Drive, Revision 3

- Maintenance Rule Scoping Document, Main Steam System, Revision 3

- Plant Health Committee Top Ten Equipment Issues, November 19, 2014

- System Health Report, Main Steam, Unit 1 and Unit 2, 3rd Quarter 2014

- Topical Report WCAP-7571, Rod Position Monitoring

- Two Year Unavailability Report, Main Steam System, Unit 1 and Unit 2, December 2, 2014

- Various 2012-2013 AMSAC System Health Reports

- Various Operator Logs, October-November 2014

- Various System Health Reports, AMSAC

1R13 Maintenance Risk Assessments and Emergent Work Control

- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7

- 12-OHP-5030-057-001, Screen House Vulnerability Determination, Revision 22

- 2-OHP-4030-219-022FV, ESW Flow Verification, Revision 18

- AR-2014-14921, 2-HV-AFP-EAC, ESW Leak

- AR-2014-14921, 2-HV-AFP-EAC, Middle Contactor Welded Shut

- AR-2014-14956, U2 West ESW Train INOP Due to Clearance Restoration

- Drawing 2-OP-5113-83, Essential Service Water

- I&C Information Change Package, ICP-00677, ESW Temperature Switches for AFW Room

Coolers, October 23, 2000

- Operating Logs, Week of November 30, 2014

- Part 1 Risk Assessments, Week of November 30, 2014

- PMP-2291-OLR-001, Online Risk Management, Revision 30

- Temporary Modification 2-TM-14-81, AFW Room Coolers

- WO 55457007-07, Install 2-TM-14-81

- WO 55457007-08, 2-HV-AFP-EAC, Perform Leak Inspection

7

1R15 Operability Determinations

- 12-EHP-5074-MOV-001, Motor Operated Valve Program, Revision 13

- 1-DCP-4894, Design Change Package for Standby Readiness Position of TDAFW Valves,

November 13, 2000- Branch Technical Position ASB 10-1, Design Guidelines for AFW System

Pump Drive and Power Supply Diversity for PWR Plants, July 1981, Revision 2

- AR 2014-13700, Unit 1 Main Steam Safety Lifted During Plant Shutdown

- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed

- AR-2014-14065, 2-FMO-222 leaks by 1%/hr, November 8, 2014

- AR-2014-7259, Question from NRC Sr. Resident still not Resolved

- AR-2014-9877 Root Cause, AB Fuel Storage Tank Alarms

- DB-12-AFWS, Auxiliary Feedwater System, Revision 5

- Draft Safety Evaluation for ICUG-001 Revision 0, NRC, May 6, 2003

- Drawing E-8708, 765kV Schematic, Revision 5

- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram

- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram

- Drawing OP-2-98101-34, Turbine Control Elementary Diagram

- EC-53931, Revise Unit 1 Ice Basket Weight Acceptance Criteria for Unit 1 Cycle 26

- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25

- FSAR Section 8.0, Electrical Systems, Revision 25

- FSAR Section 8.3, Station Service Systems, Revision 25

- Ice Condenser Utility Group Topical Report ICUG-001, Revision 3, October 23, 2003

- NRC Letter to all Operating Plants, Discussion of TMI Lessons-Learned, October 30, 1979

1R18 Plant Modifications

- AR 2014-13016, Accident Shield Requirements

- Calculation Number RS-C-0046, Doses and Dose Rates from Post LOCA Airborne Sources,

Revision 06

- Calculation Number RS-C-0171, Time Dependent Post LOCA Area by Dose Rates,

Revision 03

- Calculation Number RS-C-0232, Equipment Hatch Dose Rates - Gap Release, Revision 01

- D.C. Cook, Updated Final Safety Analysis Report (UFSAR), Several Revisions Including

Revision 23

- Engineering Calculation EC-0000049191, Units 1 and 2 Auxiliary Missile Block Removal

Project, Revision 00

- NUREG/CR-6545, Probabilistic Accident Consequences Uncertainty Analysis, Volume 2

- PMI-601, Radiation Protection Plan, Revision 20

- PNNL-14424, Health Impacts from Acute Radiation Exposure, September 2003

- PRA-DOSE-CSSEAH, Radiation Protection for Concrete Shadow Shield for Equipment

Access Hatch, Revision 00

1R19 Post-Maintenance Testing

- 12-IHP-6030-032-001, EDG Voltage Regulator Tuning and Adjustment, Revision 7

- 12-IHP-6030-IMP-063, CRID Static Inverter Transfer and Auto Retransfer Tests, Revision 8

- 12-IHP-6030-IMP-355, Check of CRID Power Supplies, Revision 9

- 12-MHP-5021-056-008, TDAFW Pump Governor Valve Maintenance, Revision 11

- 12-MHP-5021-056-011, Auxiliary Feedwater Pump Turbine Governor Maintenance, Revision 8

- 1CD EDG Aftercooler Test, 12-MHP-5021-032-015, Revision 9

- 1-OHP-4021-056-002, Auxiliary Feed Pump Operation, Revision 32

8

- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24

- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24

- 1-OHP-4024-119, Drop 29 Alarm, CRID 3 Inverter Abnormal Actions, Revision 34

- 1-OHP-4030-156-017R, AFW Pump Response Time, Revision 3

- 1-OHP-4030-156-017T, TDAFW System Test, Revision 16

- 2-EHP-6040-256-126, U2 FMO Intermediate Position High Flow Signal Test, Revision 1

- AR-2014-13672, U2 Main Generator Motored, Emergency Trip Button Pushed

- AR-2014-13724, 2-FMO-242 Went Full Open During Unit 2 Trip

- AR-2014-13730, U1 TDAFW Sentinel Valve Lifted

- AR-2014-14188, Failure in Synch Circuit for 2A7

- DB-12-AFWS, Auxiliary Feedwater System, Revision 5

- Drawing 1-OP-5106A-61, Auxiliary Feedwater

- Drawing E-8708, 765kV Schematic, Revision 5

- Drawing OP-2-5106A-55, Auxiliary Feedwater

- Drawing OP-2-98007-1, Load Tap Changer Elementary Diagram

- Drawing OP-2-98021-35, Generator and Transformer Differential Elementary Diagram

- Drawing OP-2-98101-34, Turbine Control Elementary Diagram

- EPRI Technical Report, Guidelines for Technical Evaluation of Replacement Items in Nuclear

Power Plants (NCIG-11)

- FSAR Section 7.2.3.8.14, Turbine Generator Trip, Revision 25

- FSAR Section 8.0, Electrical Systems, Revision 25

- FSAR Section 8.3, Station Service Systems, Revision 25

- Gasket Technical Data Sheets for 1CD EDG Aftercooler

- IN-86-14, PWR Auxiliary Feedwater Pump Control Problems

- IN-93-51, Repetitive Overspeed Tripping of TDAFW pumps

- Plant Computer Printouts, AFW system, November 1, 2014

- PMP-2291-PMT-001, Work Management Post-Maintenance Testing Matrices, Revision 25

- Scheduled Work, 1AB EDG, Unit 1 Fall 2014 Refueling Outage

- Terry Turbine Vendor Manual

- WO 55425039-15, Investigate Governor Valve

- WO 55432038-01, Replace 1-CRID-3-INV diodes

- WO 55455101, 2-33X-SVC-CL, Remove, Install, and PMT Relay

1R20 Outage Activities

- 12-EHP-4030-002-356, Low Power Physics Tests with Dynamic Rod Worth Measurement,

Revision 11

- 12-OHP-4021-018-002, Placing In-service the Spent Fuel Pit Cooling and Cleanup System,

Revision 27

- 12-OHP-4050-FHP-023, Reactor Vessel Head Removal with Fuel in the Vessel, Revision 11

- 1-IHP-6030-IMP-003, Adjustment of Analog RPI System, Revision 11

- 1-OHP-4021-001-002, Reactor Startup, Revision 52

- 1-OHP-4021-001-003, Power Reduction, Revision 55

- 1-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 72

- 1-OHP-4021-002-013, Reactor Coolant System Vacuum Fill, Revision 25

- 1-OHP-4021-017-002, Placing Inservice the RHR System, Revision 28

- 1-OHP-4021-082-008, Operation of CRID Power Supplies, Revision 24

- 1-OHP-4030-127-037, Refueling Surveillance, Revision 20

- 1-OHP-4030-127-041, Refueling Integrity, Revision 25

- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35

- 1-OHP-5030-001-002, Outage Risk and Technical Specification Monitoring, Revision 20

9

- 2-OHP-4021-001-002, Reactor Startup, Revision 51

- 2-OHP-4021-001-004, Plant Cooldown from Hot Standby to Cold Shutdown, Revision 60

- 2-OHP-4021-017-002, Placing Inservice the RHR System, Revision 24

- AR-2014-12738, 1-NLI-132 Reading Erroneously High, October 16, 2014

- AR-2014-13297, Lessons-learned Perform NAPRI Adjustments After Low Power,

October 23, 2014

- DIT-B-03590-00, Hot Leg Vent Size Required to Prevent RCS Pressurization During Loss of

Shutdown Cooling

- Drawing OP-1-12003-33, 250VDC One Line Diagram, Engineered Safety System

- Forced Outage Schedule, November 4, 2014

- PMP-2060-WHL-001, Work Hour Limitation and Fatigue Management, Revision 4

- PMP-4100-SDR-002, Outage Risk Assessment and Management, Revision 4

- SRP 15.7.4, Radiological Consequences of Fuel Handling Accidents, NUREG-0800

- Tagout R-4KVAC-XFM1-0184, Clearing of Unit 1 and 2 Reserve Feed

- Tagout R-CRID-CRD4-0069, 120VAC Control Room

- UFSAR Section 14.2.1.6, Radiological Consequence Analysis, Revision 25

- Unit 1 Post Trip Review Report, November 1, 2014 Trip

- Various Working Hour Records, Mechanical Maintenance, Operations, and Electrical

Maintenance Departments

1R22 Surveillance Testing

- 12-MHP-4030-010-004, Ice Condenser Intermediate Deck Door Surveillance, Revision 8

- 1-EHP-4030-128-229, Unit 1 Control Room Emergency Ventilation Surveillance,

Revision 17-18

- 1-EHP-4030-134-203, Unit 1 LLRT, Revision 16

- 1-OHP-4030-108-008R, ECCS Check Valve Test, Revision 19

- 1-OHP-4030-132-217B, DG1AB Load Sequencing and ESF Testing, Revision 35

- 50.59 Screen 2014-0469-00 for Revision 18 to 1-EHP-4030-128-229, Unit 1 Control Room

Emergency Ventilation Surveillance

- AR 2014-12787, U1 Ice Condenser Intermediate Deck Doors Exceed Opening Force

- AR-2014-11475, 1-IMO-221 Start to Open Time >2 sec

- AR-2014-11476, 1-FRV-240 Stroked too Slow for ESF test

- AR-2014-12067, Control Room Emergency Vent Outside Makeup Air Flows Low

- AR-2014-12633, N SI Pump Calculated dP high

- AR-2014-12652, South SI Pump dP High Above Action Limit

- DIT-S-06286-00, Acceptance of Normal Make Up Air Flow for Unit 1 and Unit 2 Control Room

Air Conditioning System

- Drawing OP-1-5149-48, Control Room Ventilation Unit 1

- PMP-4030-TRT-001, Time Response and Verification of Engineered Safety Features,

Revision 15

- Pump and Valve Inservice Test Program for D.C. Cook Nuclear Plant, Fourth Ten Year

Interval, Revision 1

- WO 55428831, Ice Condenser Intermediate Deck Door Surveillance, October 16, 2014

- WO 55442013-02, Perform MOV Preventive Maintenance, October 7, 2014

- WO 55453695, Ice Condenser Intermediate Deck Door Surveillance, October 18, 2014

1EP4 Emergency Action Level and Emergency Plan Changes

- AR 2014-10545, RP to Evaluate Adequacy of ERO Staffing

- AR 2014-15685, Potential EP Finding

10

- Emergency Plan, Revision 18, 19, 32, 33, 34, and 35

- PMI-2080, Emergency Plan and Implementing Procedures, Revision 18

- Safety Evaluation of Indiana Michigan Power Company Proposed Emergency Plan Changes,

March 5, 2003

2RS1 Radiological Hazard Assessment and Exposure Controls

- 12-THP-6010- RPP-104, Personnel Dosimetry Use in Varying Radiation, Revision 15

- 12-THP-6010- RPP-407, Special Radiological Evolutions, Revision 28

- 12-THP-6010-RPP-006, Radiation Work Permit Processing, Revision 34

- 12-THP-6010-RPP-314, Pressure Washing of Plant Components and Structures, Revision 8

- 12-THP-6010-RPP-401, Performance of Radiation and Contamination Surveys, Revision 36

- 12-THP-6010-RPP-405, Analysis of Airborne Radioactivity, Revision 19

- 12-THP-6010-RPP-420, Radiological Controls for Radiography, Revision 6

- 12-THP-6010-RPP-421, Radiological Controls for Steam Generator Maintenance, Revision 7

- 55399455-88, Radiography Shot Plan of Unit 1 West Containment Spray Heat Exchanger

Room and Shot Plan of Elevation 609 E/W Hallway, October 10, 2014

- AR 2013-13969, Electronic Dosimeter Setpoints Often Set Considerably Higher Than Actual or

Expected Radiological Conditions

- AR 2013-5450, Dose and Dose Rate Alarm Setpoints are Potentially too High

- AR 2014-11295, An Untrained Worker Entered the Restricted Area on the Wrong RWP

- AR 2014-11975, Dose Alarm

- AR 2014-8964, Rad Worker Deficiency

- AR 2014-9001, New Supplemental Locked High Radiation Area Ladder Cover Not Engrained

in Process

- AR 2014-9764, A Review of ED Setpoints

- CNP-1311-0001 Survey Unit 2 Upper Cavity, November 1, 2013

- CNP-1311-0012 Survey Unit 2 Upper Cavity, October 31, 2013

- PMP-6010-RPP-003, Data Sheet 4, Down Posting the Reactor Pit Area, October 16, 2014

- PMP-6010-RPP-003, High, Locked High, and Very-High Radiation Area Access, Revision 23

- PMP-6010-RPP-006, Data Sheet 2, Pre-Job ALARA Briefing Checklist, Down Post Survey of

the Rx Pit, October 16, 2014

- PMP-6010-RPP-006, Radiation Work Permit Program, Revision 19

- RWP 1 41130, U1C26 - Perform Radiography in Auxiliary & Turbine Buildings & Plant

Restricted Areas, Revision 0

- RWP 141100, U1C26 - Refuel Cavity Decontamination Activities, Revision 0

- RWP 141121, U1C26 - Auxiliary Building & Restricted Area Minor Engineering Change

Modifications and Support Work, Revision 0

- RWP 141123, Install, Remove, Modify Temporary Shielding in Unit-1 Containment, Auxiliary

Building and Plant Restricted Areas, and ALARA Plan, Revision 0

- RWP 141145, U1C26 - Valve Maintenance / Repair, Revision 2

- RWP 141148, U1C26 - Steam Generator Platform Activities, Revision 2

- RWP 141172, U1C26 - Reactor Pit VHRA Down-post Survey, Revision 0

- RWP 141187, U1C26 - Under Rx Vessel Inspections, Revision 0

- Survey SW VSDS-M-20144116-9, Critical Survey - Down Posting the Reactor Pit,

October 16, 2014

- SW_VSDS-M-20140923-1, Unit 1 Containment Spray Heat Exchanger Rooms Survey

- THG-026, Locked High Radiation Area and Very-High Radiation Weekly Verification Process,

Revision 14

- Work Order Package 55446099 01, RP Perform Semiannual Source Inventory,

August 7, 2014

11

2RS2 Occupational ALARA Planning and Controls

- ALARA Committee Meeting; A-14-33F; October 15, 2014

- D.C. Cook U1R26; ALARA Review Committee; RWP 141148 & 141149; October 15, 2014

- Full Self-Assessment Report; ALARA Program Implementation; 2014-0265; September 29, 2014

- PMP-6010-ALA-001; ALARA Program - Review of Plant Work Activities; Revision 27

2RS7 Radiological Environmental Monitoring Program

- 12 THP-6010 RPC-538, Calibration of the F&J DF-1 Low Volume Air Sampler, Revision 2

- 12 THP-6010-RPP-630, Collection of Surface Water Samples, 007

- 12 THP-6010-RPP-632, Collection of Environmental Air Samples, Revision 010

- 12 THP-6010-RPP-638, Collection of Grape and Broadleaf Samples, Revision 007

- 12 THP-6010-RPP-642, Collection of Drinking Water Samples, Revision 007

- 12-IHP-4030-036-001, Meteorological Instrumentation - Primary And Backup Towers Channel

Calibration, Revision 0

- 12-IHP-6030-036-00, Shoreline Weather Tower Instrument Calibration, Revision 000

- 12-THP-6020-INS-525, Liquid Scintillation Counter, Revision 009

- 12-THP-6020-INS-526, Gamma Spectrometry Using Ortec Global Value and Gamma Vision

Software, Revision 002

- 2013 Radiological Environmental Monitoring Program Land Use Census, September 24, 2013

- Annual Radiological Environmental Operating Report, Donald C. Cook Nuclear Plant

Radiological Environmental Monitoring Program, January 1, 2013 - December 31, 2013

- AR 2013-10179, ONS-5 Air Station Was Out of Service for Approximately 37.5 Hours

- AR 2013-15116, MET Tower Data Recovery

- AR 2013-3738, Quarterly Radiological Environmental Monitoring Program (REMP) TLD

Collection and Change Out, TLD T-11 Could Not Be Located

- AR 2013-6824, ONS-1 Air Station was Out of Service for Approximately 2.5 Hours

- AR 2013-7934, COL (Coloma) Air Station was Out of Service For Approximately 0.5 Hours

- AR 2014-10063, 12-ELR-400, East Bucket Heater Broken

- AR 2014-11607, Environmental Technician was Notified That the Control Farm Would No

Longer Produce Milk

- AR 2014-13656, Trace Cesium-137 in Broadleaf Sample

- AR 2014-5725, First Quarter of 2014, With The Exception Of Two Days (March 23 And 24),

Ice Build Up On Lake Michigan Prevented the Collection of Radiological Environmental

Monitoring Program (REMP) Surface Water Samples,

- AR 2014-6725 Radiological Environmental Monitoring Program (REMP) Air Station ONS-1

Lost Power for Approximately 39 minutes

- AR 2014-8378, Document Results Of The Weekly Review Of Radiological Environmental

Monitoring Program (REMP) Data

- AR 2014-8622, Primary Met Tower Carriage Control Switch

- AR2013-12672, Evaluate Siting of ONS-2 and ONS-6

- D. C. Cook Nuclear Plant Updated Final Safety Analysis Report, Section 11.0, Waste Disposal

and Radiation Protection System, Revision 25.0

- PA-13-01, Performance Assurance Audit, Radiological Environmental Monitoring Program and

Offsite Dose Calculation Manual, March 1, 2013

- PMP-6010-OSD-001, Off-Site Dose Calculation Manual, Revision 24

- WO 554444469, Meteorological Instrumentation Calibration, October 11, 2014

12

4OA1 Performance Indicator Verification

- Dose Calculations and Dose Projections Due to Liquid and Gaseous Effluents for D.C. Cook

Plant, July, 2013 to September 14, 2014

- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly

Operation Report Data, Reactor Coolant System Specific Activity, Revision 15

- PMP-7110-PIP-001, Reactor Oversight Program Performance Indicators and Monthly

Operating Report Data, Revision 15

4OA2 Identification and Resolution of Problems

- 12-OHP-4025-001-002, Fire Response Guidelines, Revision 6

- AR 2014-11148, Worker Bumped Detector 3-12 Sends Fire Alarm to U-1 Control Room

- AR 2014-9531, 1-152-CICE4-2A Out of Position

- AR-2012-8187, Adequacy of Past Operability Questioned

- AR-2013-8600, Fire Zone 79 EDG Corridor Fire with Simultaneous CO2 Actuation

- AR-2013-9251, Inadequate Calculations for ICP-0083 Revision 0 12-ZPS-411

- AR-2014-10600, Difference Between Fire Pump Performance in Hydraulic Calcs

- AR-2014-14920, Racking Interlocks Potential to not Properly Reset

- AR-2014-14951, Primary Coolant Filters Wrong Parts

- AR-2014-15040, Missing Sheet Metal Screws on Room Cooler Housing

- AR-2014-15059, Cable 2-8167G Low Megger Readings

- AR-2014-15087, Fire Pump Setpoint and New TRM Sprinkler Demand

- GT-2014-11170-3, Work Order Task Package Quality QHSA Report, October 30, 2014

- Performance Assurance Audit PA-14-07, Operations, August 25, 2014

- Performance Assurance Quarterly Report, April - June 2014

- Performance Assurance Quarterly Report, July - September 2014

- Performance Assurance Surveillance, PA-SA-14-001, U1C26 Refueling Outage,

November 3, 2014

- Unit 1 and Unit 2 Contingency/Compensatory Actions, December 4, 2014

- Unit 1 and Unit 2 Operator Burden Report, November 18, 2014 and December 4, 2014

- Unit 1 and Unit 2 Supervisor Turnover Checklist, December 4, 2014

4OA3 Identification and Resolution of Problems

- 12-OHP-4022-057-001, Screen House Forebay Degraded Condition, Revision 7

- AR 2014-13669 Task 2, Unit 1 Post-trip Report

- AR 2014-13669 Task 3, Unit 2 Post-trip Report

- E-0, Reactor Trip or Safety Injection, Revision 38

- ES-0.1, Reactor Trip Response, Revision 28

- Ltr Lee Baun to Cook Leadership, Performance Assurance Semi-Monthly Roll-Up Report,

December 22, 2014

13

LIST OF ACRONYMS USED

ADAMS

Agencywide Document Access Management System

AFW

Auxiliary Feedwater

ALARA

As-Low-As-Reasonably-Achievable

AMB

Auxiliary Missile Blocks

AR

Action Request

ASME

American Society for Mechanical Engineers

BACC

Boric Acid Corrosion Control

CAP

Corrective Action Program

CAQ

Condition Adverse to Quality

CDF

Core Damage Frequency

CFR

Code of Federal Regulations

dpm

drops per minute

EAC

Environmental Assessment Coordinator

EDG

Emergency Diesel Generator

EPRI

Electric Power Research Institute

ET

Eddy Current

FME

Foreign Material Exclusion

FOST

Fuel Oil Storage Tank

ISI

Inservice Inspection

LBLOCA

Large Break Loss-of-Coolant Accident

LHRA

Locked High Radiation Area

LOCA

Loss-of-Coolant Accident

IMC

Inspection Manual Chapter

IP

Inspection Procedure

IR

Inspection Report

LCO

Limiting Condition for Operation

MDAFW

Motor-Driven Auxiliary Feedwater

MSPI

Mitigating Systems Performance Index

NCV

Non- Violation

NDE

Non-destructive Examination

NEI

Nuclear Energy Institute

NRC

U.S. Nuclear Regulatory Commission

PARS

Publicly Available Records System

PI

Performance Indicator

RAC

Radiological Assessment Coordinator

RCS

Reactor Coolant System

RG

Regulatory Guide

RPT

Radiation Protection Technician

SDP

Significance Determination Process

SG

Steam Generator

SRA

Senior Reactor Analyst

SSC

Structure, System and Component

TDAFW

Turbine-Driven Auxiliary Feedwater

TS

Technical Specification

14

TTV

Trip and Throttle Valve

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

UT

Ultrasonic Test

WO

Work Order

L. Weber

-2-

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy

of this letter, its enclosure, and your response (if any) will be available electronically for public

inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS)

component of the NRC's Agencywide Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief

Branch 2

Division of Reactor Projects

Docket Nos. 50-315; 50-316

License Nos. DPR-58; DPR-74

Enclosure:

IR 05000315/2014005; 05000316/2014005

w/Attachment: Supplemental Information

cc w/encl: Distribution via LISTSERV

DISTRIBUTION w/encl:

Kimyata MorganButler

RidsNrrDorlLpl3-1 Resource

RidsNrrPMDCCook Resource

RidsNrrDirsIrib Resource

Cynthia Pederson

Darrell Roberts

Eric Duncan

Allan Barker

Carole Ariano

Linda Linn

DRPIII

DRSIII

Jim Clay

Carmen Olteanu

ROPreports.Resource@nrc.gov

ADAMS Accession Number:

Publicly Available

Non-Publicly Available

Sensitive

Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII-EICS

RIII

RIII

NAME

NS:rj

PLougheed for

EDuncan

KRiemer

DATE

02/09/15

02/09/15

02/10/15

OFFICIAL RECORD COPY