Information Notice 1997-21, Availability of Alternate AC Power Source Designed for Station Blackout Event: Difference between revisions

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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES


NUCLEAR REGULATORY COMMISSION
===NUCLEAR REGULATORY COMMISSION===
OFFICE OF NUCLEAR REACTOR REGULATION


OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555-0001


WASHINGTON, D.C. 20555-0001 April 18, 1997 NRC INFORMATION NOTICE 97-21:               AVAILABILITY OF ALTERNATE AC POWER
===April 18, 1997===
NRC INFORMATION NOTICE 97-21:  


===AVAILABILITY OF ALTERNATE AC POWER===
SOURCE DESIGNED FOR STATION BLACKOUT
SOURCE DESIGNED FOR STATION BLACKOUT


Line 77: Line 80:


PDRA X4-E 06rICE 7T-Ozf T7vq18
PDRA X4-E 06rICE 7T-Ozf T7vq18
                                                                  1INlpiglpig PIlllstl~lll
1INlpiglpig PIlllstl~lll


IN 97-21 April 18, 1997 DG support systems, particularly the lubricating oil system, was powered by a nonsafety- related power supply and had been out for an extended period during the loss of offsite
IN 97-21 April 18, 1997 DG support systems, particularly the lubricating oil system, was powered by a nonsafety- related power supply and had been out for an extended period during the loss of offsite
Line 95: Line 98:
offsite power) following a postulated LOOP event.
offsite power) following a postulated LOOP event.


The Pilgrim licensee discovered that the SBO DC was susceptible to a failure to start as a
The Pilgrim licensee discovered that the SBO DC
 
was susceptible to a failure to start as a


result of low oil temperature if power was lost to the lubricating oil keep-warm system for an
result of low oil temperature if power was lost to the lubricating oil keep-warm system for an


extended period. The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes, or modifications to SBO DG start logic.
extended period.
 
The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes, or modifications to SBO DG start logic.


The SBO DG capability to start on demand depends on the availability of the necessary
The SBO DG capability to start on demand depends on the availability of the necessary
Line 123: Line 130:
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.


Thomas T. Martin, Director
===Thomas T. Martin, Director===
 
Division of Reactor Program Management
Division of Reactor Program Management


Office of Nuclear Reactor Regulation
===Office of Nuclear Reactor Regulation===
Technical contacts:
A. Pal, NRR


Technical contacts:      A. Pal, NRR                                David Skeen
David Skeen


(301) 415-2760                             (301) 415-1174 E-mail: anpenrc.gov                        E-mail: dlsenrc.gov
(301) 415-2760  
(301) 415-1174 E-mail: anpenrc.gov


Thomas Koshy
E-mail: dlsenrc.gov


===Thomas Koshy===
(301) 415-1176 E-mail: txkenrc.gov
(301) 415-1176 E-mail: txkenrc.gov


Attachment: List of Recently Issued NRC Information Notices
Attachment: List of Recently Issued NRC Information Notices


4+,q¢ Mivr               -QfeLD A         )Ct
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<-IJ
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Attachment 1 IN 97-21 April 18, 1997 LIST OF RECENTLY ISSUED
===Attachment 1===
IN 97-21


===April 18, 1997 LIST OF RECENTLY ISSUED===
NRC INFORMATION NOTICES
NRC INFORMATION NOTICES


Information                                       Date of
Information
 
Date of


Notice No.           Subject                    Issuance    Issued to
Notice No.


97-20          Identification of                04/18'97    All holders of OLs
Subject


Certain Uranium                              for nuclear power
Issuance


Hexafluoride Cylinders
Issued to


97-20
97-19
94-14, Supp. 1
97-18
97-17
===Identification of===
Certain Uranium
===Hexafluoride Cylinders===
that do not comply
that do not comply


Line 163: Line 193:
Standards
Standards


97-19          Safaty Injection                 04/1 8,'/7  All holders of OLs
===Safaty Injection===
System Weld Flaw at


System Weld Flaw at                          or CPs for nuclear
===Sequoyah Nuclear===
Power Plant, Unit 2
 
===Failure to Implement===
Requirements for
 
===Biennial Medical===
Examinations and
 
===Notification to the===
NRC of Changes in
 
===Licensed Operator===
Medical Conditions
 
===Problems Identified===
During Maintenance
 
===Rule Baseline Inspections===
Cracking of Vertical
 
===Welds in the Core===
Shroud and Degraded


Sequoyah Nuclear                              power reactors
Repair


Power Plant, Unit 2
04/18'97
94-14,          Failure to Implement            04/14/97   All holders of OLs
04/1 8,'/7
04/14/97
04/14/97
04/04/97


Supp. 1          Requirements for                            or CPs for nuclear
===All holders of OLs===
for nuclear power


Biennial Medical                            power and non-power
===All holders of OLs===
or CPs for nuclear


Examinations and                              reactors and all
power reactors


Notification to the                          licensed reactor
===All holders of OLs===
or CPs for nuclear


NRC of Changes in                            operators and senior
power and non-power


Licensed Operator                            reactor operators
reactors and all


Medical Conditions
licensed reactor


97-18          Problems Identified              04/14/97    All holders of OLs, During Maintenance                            CPs, and decommissioning- Rule Baseline Inspections                    stage licenses for
operators and senior


nuclear power reactors
reactor operators


97-17          Cracking of Vertical              04/04/97    All holders of OLs
All holders of OLs, CPs, and decommissioning- stage licenses for


Welds in the Core                            or CPs for boiling- Shroud and Degraded                          water reactors
nuclear power reactors


Repair
===All holders of OLs===
or CPs for boiling- water reactors


OL = Operating License
OL = Operating License
Line 220: Line 280:
result of low oil temperature if power was lost to the lubricating oil keep-warm system for an
result of low oil temperature if power was lost to the lubricating oil keep-warm system for an


extended period. The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes, or modifications to SBO DG start logic.
extended period.
 
The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes, or modifications to SBO DG start logic.


The SBO DG capability to start on demand depends on the availability of the necessary
The SBO DG capability to start on demand depends on the availability of the necessary
Line 244: Line 306:
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.


Thomas T. Martin, Director
===Thomas T. Martin, Director===
 
Division of Reactor Program Management
Division of Reactor Program Management


Office of Nuclear Reactor Regulation
===Office of Nuclear Reactor Regulation===
Technical contacts:
A. Pal, NRR


Technical contacts:      A. Pal, NRR                                          David Skeen
David Skeen


(301) 415-2760                                       (301) 415-1174 E-mail: anp@nrc.gov                                  E-mail: dls@nrc.gov
(301) 415-2760  
(301) 415-1174 E-mail: anp@nrc.gov


Thomas Koshy
E-mail: dls@nrc.gov


===Thomas Koshy===
(301) 415-1176 E-mail: txk@nrc.gov
(301) 415-1176 E-mail: txk@nrc.gov


Attachment: List of Recently Issued NRC Information Notices
Attachment: List of Recently Issued NRC Information Notices


DOCUMENT NAME: S:\DRPMSEC\97-21.lN                         *SEE PREVIOUS CONCURRENCES
DOCUMENT NAME: S:\\DRPMSEC\\97-21.lN
 
*SEE PREVIOUS CONCURRENCES
 
To receive a copy of Us document, Indicate In the box:
V' a Copy without enclosures "E" c Copy with enlosures "N"
No copy


To receive a copy of Us document, Indicate In the box:  V' a Copy without enclosures "E" c Copy with enlosures "N" No copy
OFFICE


OFFICE        TECH
TECH


==CONTACT==
==CONTACT==
S             C:EELB                 CPECB                     D:DRPMl
S
 
C:EELB
 
CPECB
 
D:DRPMl
 
NAME


NAME          APa1*                     JCalvo*                 AChaffee*                 T~artin
APa1*  
JCalvo*  
AChaffee*  
T~artin


DSkeen*_
DSkeen*_
DATE         04/07/97                   04/07/97               04/11/97                 04/       97 OFFICIAL RECORD COPY
DATE
 
04/07/97  
04/07/97  
04/11/97  
04/  
97
 
===OFFICIAL RECORD COPY===


IN 97 -xx
IN 97 -xx
Line 318: Line 408:
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.


Thomas T. Martin, Director
===Thomas T. Martin, Director===
 
Division of Reactor Program Management
Division of Reactor Program Management


Office of Nuclear Reactor Regulation
===Office of Nuclear Reactor Regulation===
Technical contacts:
A. Pal, NRR


Technical contacts:        A. Pal, NRR                                          David Skeen
David Skeen


(301) 415-2760                                       (301) 415-1174 E-mail: anp@nrc.gov                                  E-mail: dls@nrc.gov
(301) 415-2760  
(301) 415-1174 E-mail: anp@nrc.gov


Thomas Koshy
E-mail: dls@nrc.gov


===Thomas Koshy===
(301) 415-1176 E-mail: btk@nrc.gov
(301) 415-1176 E-mail: btk@nrc.gov


Attachment: List of Recently Issued NRC Information Notices
Attachment: List of Recently Issued NRC Information Notices


DOCUMENT NAME: G:%TXKXSBO.3                                   *SEE PREVIOUS CONCURRENCES
DOCUMENT NAME: G:%TXKXSBO.3  
*SEE PREVIOUS CONCURRENCES
 
To receive a copy of this document, Indicate In the box: "C' = Copy wftiout enclosures "E - Copy with enclosures "N"
No copy


To receive a copy of this document, Indicate In the box: "C' = Copy wftiout enclosures "E - Copy with enclosures "N" No copy
OFFICE


OFFICE        TECH
TECH


==CONTACT==
==CONTACT==
S                   I       IC:EELB     C             I         D: DRPM
S
 
I
 
IC:EELB
 
C
 
I
 
D: DRPM
 
NAME


NAME          APal*                       JCalvo*                 AChaffee*               TMartin
APal*  
JCalvo*  
AChaffee*  
TMartin


TKoshy
TKoshy


DSkeen*
DSkeen*
DATE         04/07/97                     04/07/97               04/11/97                 04/     /97 OFFICIALTRECOR C/OPI
DATE
 
04/07/97  
04/07/97  
04/11/97  
04/ /97 OFFICIALTRECOR
 
I
 
C/OP


4 fX' q11V?7
4 fX' q11V?7


*                                                             lN 97 -xx
*  
lN 97 -xx


April xx, 1997 safety related power supply and had been out for an extended period during the loss of
April xx, 1997 safety related power supply and had been out for an extended period during the loss of
Line 374: Line 496:
result of low oil temperature if power was lost to the lubricating oil keep-warm system for an
result of low oil temperature if power was lost to the lubricating oil keep-warm system for an


extended period. The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes or modifications to SBO DG start logic.
extended period.
 
The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes or modifications to SBO DG start logic.


The SBO DG capability to start on demand depends on the availability of the necessary
The SBO DG capability to start on demand depends on the availability of the necessary
Line 398: Line 522:
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.
listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.


Thomas T. Martin, Director
===Thomas T. Martin, Director===
 
Division of Reactor Program Management
Division of Reactor Program Management


Office of Nuclear Reactor Regulation
===Office of Nuclear Reactor Regulation===
Technical Contacts: A. Pal, NRR


Technical Contacts: A. Pal, NRR                              Thomas Koshy David Skeen
Thomas Koshy


(301) 415-2760                   (301) 415-1176 (301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV
David Skeen
 
(301) 415-2760  
(301) 415-1176  
(301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV


Attachment: List of Recently Issued NRC Information Notices
Attachment: List of Recently Issued NRC Information Notices


DOCUMENT NAME: G:%TXKMSBO.3 To receive a copy of this document, Indicate In the box: "CT a Copy without enclosures "'Fn Copy with enclosures "N'u No copy
DOCUMENT NAME: G:%TXKMSBO.3 To receive a copy of this document, Indicate In the box: "CT a Copy without enclosures "'F


OFFICE       TECH
n Copy with enclosures "N'
u No copy
 
OFFICE
 
TECH


==CONTACT==
==CONTACT==
S I               :EELB       T         C:PECB                lm DI                IPIM
S I
 
:EELB
 
T


NAME         APal*                       JCalvo*                 AChaffee                 TMartin
C:PECB
 
lm DI
 
IPIM
 
NAME
 
APal*  
JCalvo*  
AChaffee
 
TMartin


TKoshy
TKoshy


DSkeen*
DSkeen*
DATE         04/07/97                     04/07/97                 04,1/97                 104/     /97 OFFICIAL RECORD COPY
DATE
 
04/07/97  
04/07/97  
04,1/97  
104/  
/97
 
===OFFICIAL RECORD COPY===
 
*.


*.                                                                            I"7 -xx
I"7  
-xx


March xx, 1997 safety related power supply and had been out for an extended period during the loss of
March xx, 1997 safety related power supply and had been out for an extended period during the loss of
Line 446: Line 606:
result of low oil temperature if power was lost to the lubricating oil keep-warm system for
result of low oil temperature if power was lost to the lubricating oil keep-warm system for


an extended period. The licensee is considering enhanced monitoring of SBO DG
an extended period.
 
The licensee is considering enhanced monitoring of SBO DG


auxiliaries, procedural changes or modifications to SBO DG start logic.
auxiliaries, procedural changes or modifications to SBO DG start logic.
Line 474: Line 636:
manager.
manager.


Thomas T. Martin, Director
===Thomas T. Martin, Director===
Division of Reactor Program Management


Division of Reactor Program Management
===Office of Nuclear Reactor Regulation===
Technical Contacts: A. Pal, NRR


Office of Nuclear Reactor Regulation
Thomas Koshy


Technical Contacts: A. Pal, NRR                          Thomas Koshy David Skeen
David Skeen


(301) 415-2760               (301) 415-1176 (301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV
(301) 415-2760  
(301) 415-1176 (301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV


Attachment: List of Recently Issued NRC Information Notices
Attachment: List of Recently Issued NRC Information Notices


DOCUMENT NAME: G:\TXK\SBO.3 To receive a copy of this document. Indicate Inthe box: Ca- Copy without enclosures E - Copy with enclosures EN" = No copy
DOCUMENT NAME: G:\\TXK\\SBO.3 To receive a copy of this document. Indicate In the box:  
Ca- Copy without enclosures


IOFFICE         TECH
E - Copy with enclosures
 
EN" = No copy
 
IOFFICE
 
TECH


==CONTACT==
==CONTACT==
S                 C:EELB             C:PECB                 D:DRPM
S
 
C:EELB
 
C:PECB
 
D:DRPM
 
NAME
 
APa1*
JCalvo*
AChaffee


NAME          APa1*                        JCalvo*              AChaffee                TMartin
TMartin


TKoshy A
TKoshy A


DSkeen*
DSkeen*
DATE         1046997               /97     04/      04/ /97                         104/ /97 OFFICIAL RECORD WPY7
DATE
 
1046997  
04/
/97  
04/  
/97  
104/ /97
 
===OFFICIAL RECORD WPY7===


I 1W7-xx
I 1W7-xx
Line 522: Line 715:
result of low oil temperature if power was lost to the lubricating oil keep-warm system for
result of low oil temperature if power was lost to the lubricating oil keep-warm system for


an extended period. The licensee is considering enhanced monitoring of SBO DG
an extended period.
 
The licensee is considering enhanced monitoring of SBO DG


auxiliaries, procedural changes or modifications to SBO DG start logic.
auxiliaries, procedural changes or modifications to SBO DG start logic.
Line 550: Line 745:
manager.
manager.


Thomas T. Martin, Director
===Thomas T. Martin, Director===
Division of Reactor Program Management


Division of Reactor Program Management
===Office of Nuclear Reactor Regulation===
Technical Contacts: A. Pal, NRR


Office of Nuclear Reactor Regulation
Thomas Koshy


Technical Contacts: A. Pal, NRR                              Thomas Koshy David Skeen
David Skeen


(301) 415-2760                   (301) 415-1176 (301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV
(301) 415-2760  
(301) 415-1176 (301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV


Attachment: List of Recently Issued NRC Information Notices
Attachment: List of Recently Issued NRC Information Notices


DOCUMENT NAME: G:\TXK\SBO.3 To receive a copy of this document, Indicate in the box: 'C' - Copy without enclosures 'E" - Copy with enclosures   N - No copy
DOCUMENT NAME: G:\\TXK\\SBO.3 To receive a copy of this document, Indicate in the box: 'C' - Copy without enclosures
 
'E" - Copy with enclosures
 
N - No copy
 
OFFICE


OFFICE        TECH
TECH


==CONTACT==
==CONTACT==
S I                 IC:EELB       TI     C:PECB           I     ID:DRPM             I
S I
 
IC:EELB
 
TI
 
C:PECB
 
I
 
ID:DRPM
 
I
 
NAME


NAME          APa1*                         JCalvo*               AChaffee                 TMartin
APa1*  
JCalvo*  
AChaffee
 
TMartin


7Koshy
7Koshy
oats


DSkeen*_
DSkeen*_
                          oats
DATE


DATE          04/? /97                       04/     /97           04/ /97                   04/     /97 OFFICIAL RECORD COPY}}
04/? /97  
04/  
/97  
04/  
/97  
04/  
/97 OFFICIAL RECORD COPY}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 10:56, 16 January 2025

Availability of Alternate AC Power Source Designed for Station Blackout Event
ML031050325
Person / Time
Site: Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant, Crane  Entergy icon.png
Issue date: 04/18/1997
From: Martin T
Office of Nuclear Reactor Regulation
To:
References
IN-97-021, NUDOCS 9704180103
Download: ML031050325 (8)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001

April 18, 1997

NRC INFORMATION NOTICE 97-21:

AVAILABILITY OF ALTERNATE AC POWER

SOURCE DESIGNED FOR STATION BLACKOUT

EVENT

Addressees

All holders of operating licenses for nuclear power reactors.

Purpose

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to alert

addressees to potential unavailability of an alternate ac (AAC) power source during a station

blackout (SBO) event. It is expected that recipients will review this information for

applicability to their facilities and consider actions, as appropriate, to avoid similar problems.

However, suggestions contained in this information notice are not NRC requirements;

therefore, no specific action or written response is required.

Description of Circumstances

On March 11-29, and May 13-22, 1996, a special inspection team from the NRC assessed

the engineering and licensing activities at Millstone Nuclear Power Station. During a review

of the Millstone Unit 3 SBO systems, the team identified a concern about the design of the

AAC power source, the SBO diesel generator (DG), and its dedicated battery. The AAC

power source may not be available if an SBO occurs as a result of a loss of onsite power, i.e., the EDGs, following 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of loss of offsite (preferred) power (LOOP). The AAC power

source at Millstone Unit 3 is controlled and monitored by a computer. The AAC power

system includes two batteries, one 48-volt battery for the computer and one 125-volt battery

for DG field flashing, oil pump, and breaker control power. The battery chargers for these

batteries are fed from offsite power when the AAC power is not operating. If offsite power is

lost for a significant period, these batteries will be depleted as a result of the connected loads

(the computer for the 48-volt battery and the EDG oil pump for the 125-volt battery). If AAC

power is needed more than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> after the loss of offsite power, the batteries will be so

depleted that the SBO DG cannot be started and therefore, will not be available if EDGs are

lost.

On March 7, 1997, during a refueling outage at Pilgrim Unit 1 a main transformer failure

resulted in both safety buses losing power. One safety bus was energized from the

shutdown transformer and the other from EDG "B." Approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> into the event, operators attempted to start the SBO DG, but failed. The SBO-DG failed to start because the

PDRA X4-E 06rICE 7T-Ozf T7vq18

1INlpiglpig PIlllstl~lll

IN 97-21 April 18, 1997 DG support systems, particularly the lubricating oil system, was powered by a nonsafety- related power supply and had been out for an extended period during the loss of offsite

power. This extended loss of auxiliary power caused the oil temperature to drop and that

resulted in oil pressure below the minimum pressure required for DG operation.

Discussion

The Millstone licensee reviewed the design and operation of the MC power source at

Millstone Unit 3 and determined that the MC power source required modification to assure

availability of the SBO DG for no less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (the probable time needed to restore

offsite power) following a postulated LOOP event.

The Pilgrim licensee discovered that the SBO DC

was susceptible to a failure to start as a

result of low oil temperature if power was lost to the lubricating oil keep-warm system for an

extended period.

The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes, or modifications to SBO DG start logic.

The SBO DG capability to start on demand depends on the availability of the necessary

support systems to fulfill their required function. The SBO DG support systems may require

varying combinations of dc or ac power for varying periods to maintain operational readiness.

Prompt operator actions to conserve battery capacity, support system power supply

modifications, use of special procedures, or start logic modifications may be necessary to

preserve the operational readiness of the SBO DG under challenging environmental

conditions. The staff is evaluating these events and the consequential need for additional

generic communications.

This information notice requires no specific action or written response. If you have any

questions about the .nformation in this notice, please contact one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.

Thomas T. Martin, Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts:

A. Pal, NRR

David Skeen

(301) 415-2760

(301) 415-1174 E-mail: anpenrc.gov

E-mail: dlsenrc.gov

Thomas Koshy

(301) 415-1176 E-mail: txkenrc.gov

Attachment: List of Recently Issued NRC Information Notices

4+,q¢ Mivr

-QfeLD

A

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<-IJ

Attachment 1

IN 97-21

April 18, 1997 LIST OF RECENTLY ISSUED

NRC INFORMATION NOTICES

Information

Date of

Notice No.

Subject

Issuance

Issued to

97-20

97-19

94-14, Supp. 1

97-18

97-17

Identification of

Certain Uranium

Hexafluoride Cylinders

that do not comply

with ANSI N14.1 Fabrication

Standards

Safaty Injection

System Weld Flaw at

Sequoyah Nuclear

Power Plant, Unit 2

Failure to Implement

Requirements for

Biennial Medical

Examinations and

Notification to the

NRC of Changes in

Licensed Operator

Medical Conditions

Problems Identified

During Maintenance

Rule Baseline Inspections

Cracking of Vertical

Welds in the Core

Shroud and Degraded

Repair

04/18'97

04/1 8,'/7

04/14/97

04/14/97

04/04/97

All holders of OLs

for nuclear power

All holders of OLs

or CPs for nuclear

power reactors

All holders of OLs

or CPs for nuclear

power and non-power

reactors and all

licensed reactor

operators and senior

reactor operators

All holders of OLs, CPs, and decommissioning- stage licenses for

nuclear power reactors

All holders of OLs

or CPs for boiling- water reactors

OL = Operating License

CP = Construction Permit

IN 97-21 April 18,1997 DG support systems, particularly the lubricating oil system, was powered by a nonsafety- related power supply and had been out for an extended period during the loss of offsite

power. This extended loss of auxiliary power caused the oil temperature to drop and that

resulted in oil pressure below the minimum pressure required for DG operation.

Discussion

The Millstone licensee reviewed the design and operation of the MC power source at

Millstone Unit 3 and determined that the AAC power source required modification to assure

availability of the SBO DG for no less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (the probable time needed to restore

offsite power) following a postulated LOOP event.

The Pilgrim licensee discovered that the SBO DG was susceptible to a failure to start as a

result of low oil temperature if power was lost to the lubricating oil keep-warm system for an

extended period.

The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes, or modifications to SBO DG start logic.

The SBO DG capability to start on demand depends on the availability of the necessary

support systems to fulfill their required function. The SBO DG support systems may require

varying combinations of dc or ac power for varying periods to maintain operational readiness.

Prompt operator actions to conserve battery capacity, support system power supply

modifications, use of special procedures, or start logic modifications may be necessary to

preserve the operational readiness of the SBO DG under challenging environmental

conditions. The staff is evaluating these events and the consequential need for additional

generic communications.

This information notice requires no specific action or written response. If you have any

questions about the information in this notice, please contact one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.

Thomas T. Martin, Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts:

A. Pal, NRR

David Skeen

(301) 415-2760

(301) 415-1174 E-mail: anp@nrc.gov

E-mail: dls@nrc.gov

Thomas Koshy

(301) 415-1176 E-mail: txk@nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: S:\\DRPMSEC\\97-21.lN

  • SEE PREVIOUS CONCURRENCES

To receive a copy of Us document, Indicate In the box:

V' a Copy without enclosures "E" c Copy with enlosures "N"

No copy

OFFICE

TECH

CONTACT

S

C:EELB

CPECB

D:DRPMl

NAME

APa1*

JCalvo*

AChaffee*

T~artin

DSkeen*_

DATE

04/07/97

04/07/97

04/11/97

04/

97

OFFICIAL RECORD COPY

IN 97 -xx

April xx, 1997 DG support systems, particularly the lubricating oil system, was powered by a nonsafety- related power supply and had been out for an extended period during the loss of offsite

power. This extended loss of auxiliary power caused the oil temperature to drop and that

resulted in oil pressure below the minimum pressure required for DG operation.

Discussion

The Millstone licensee reviewed the design and operation of the MC power source at

Millstone Unit 3 and determined that the AAC power source required modification to assure

availability of the SBO DG for no less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (the probable time needed to restore

offsite power) following a postulated LOOP event.

The Pilgrim licensee discovered that the SBO DG was susceptible to a failure to start as a

result of low oil temperature if power was lost to the lubricating oil keep-warm system for an

extended period. The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes, or modifications to SBO DG start logic.

The SBO DG capability to start on demand depends on the availability of the necessary

support systems to fulfill their required function. The SBO DG support systems may require

varying combinations of dc or ac power for varying periods to maintain operational readiness.

Prompt operator actions to conserve battery capacity, support system power supply

modifications, use of special procedures, or start logic modifications may be necessary to- preserve the operational readiness of the SBO DG under challenging environmental

conditions. The staff is evaluating these events and the consequential need for additional

generic communications.

This information notice requires no specific action or written response. If you have any

questions about the information in this notice, please contact one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.

Thomas T. Martin, Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts:

A. Pal, NRR

David Skeen

(301) 415-2760

(301) 415-1174 E-mail: anp@nrc.gov

E-mail: dls@nrc.gov

Thomas Koshy

(301) 415-1176 E-mail: btk@nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:%TXKXSBO.3

  • SEE PREVIOUS CONCURRENCES

To receive a copy of this document, Indicate In the box: "C' = Copy wftiout enclosures "E - Copy with enclosures "N"

No copy

OFFICE

TECH

CONTACT

S

I

IC:EELB

C

I

D: DRPM

NAME

APal*

JCalvo*

AChaffee*

TMartin

TKoshy

DSkeen*

DATE

04/07/97

04/07/97

04/11/97

04/ /97 OFFICIALTRECOR

I

C/OP

4 fX' q11V?7

lN 97 -xx

April xx, 1997 safety related power supply and had been out for an extended period during the loss of

offsite power. This extended loss of auxiliary power caused the oil temperature to drop and

that resulted in oil pressure below the minimum pressure required for DG operation.

Discussion

The Millstone licensee reviewed the design and operation of the AAC power source at

Millstone Unit 3 and determined that the AAC power source required modification to assure

availability of the SBO DG for no less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (the probable time needed to restore

offsite power) following a postulated LOOP event.

The Pilgrim licensee discovered that the SBO DG was susceptible to a failure to start as a

result of low oil temperature if power was lost to the lubricating oil keep-warm system for an

extended period.

The licensee is considering enhanced monitoring of SBO DG auxiliaries, procedural changes or modifications to SBO DG start logic.

The SBO DG capability to start on demand depends on the availability of the necessary

support systems to fulfill their required function. The SBO DG support systems may require

varying combinations of dc or ac power for varying periods to maintain operational readiness.

Prompt operator actions to conserve battery capacity, support system power supply

modifications, use of special procedures, or start logic modifications may be necessary to

preserve the operational readiness of the SBO DG under challenging environmental

conditions. The staff is evaluating these events and the consequential need for additional

generic communications.

This information notice requires no specific action or written response. If you have any

questions about the information in this notice, please contact one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager.

Thomas T. Martin, Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical Contacts: A. Pal, NRR

Thomas Koshy

David Skeen

(301) 415-2760

(301) 415-1176

(301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:%TXKMSBO.3 To receive a copy of this document, Indicate In the box: "CT a Copy without enclosures "'F

n Copy with enclosures "N'

u No copy

OFFICE

TECH

CONTACT

S I

EELB

T

C:PECB

lm DI

IPIM

NAME

APal*

JCalvo*

AChaffee

TMartin

TKoshy

DSkeen*

DATE

04/07/97

04/07/97

04,1/97

104/

/97

OFFICIAL RECORD COPY

  • .

I"7

-xx

March xx, 1997 safety related power supply and had been out for an extended period during the loss of

offsite power. This extended loss of auxiliary power caused the oil temperature to drop

and that resulted in oil pressure below the minimum pressure required for DG operation.

Discussion

The Millstone licensee reviewed the design and operation of the AAC power source at

Millstone Unit 3 and determined that the AAC power source required modification to

assure availability of the SBO DG for no less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (the probable time needed to

restore offsite power) following a postulated LOOP event.

The Pilgrim licensee discovered that the SBO DG was susceptible to a failure to start as a

result of low oil temperature if power was lost to the lubricating oil keep-warm system for

an extended period.

The licensee is considering enhanced monitoring of SBO DG

auxiliaries, procedural changes or modifications to SBO DG start logic.

The SBO DG capability to start on demand depends on the availability of the necessary

support systems to fulfill their required function. The SBO DG support systems may

require varying combinations of dc or ac power for varying periods to maintain operational

readiness. Prompt operator actions to conserve battery capacity, support system power

supply modifications, use of special procedures, or start logic modifications may be

necessary to preserve the operational readiness of the SBO DG under challenging

environmental conditions. The staff is evaluating these events and the consequential need

for additional generic communications.

This information notice requires no specific action or written response. If you have any

questions about the information in this notice, please contact one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project

manager.

Thomas T. Martin, Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical Contacts: A. Pal, NRR

Thomas Koshy

David Skeen

(301) 415-2760

(301) 415-1176 (301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\\TXK\\SBO.3 To receive a copy of this document. Indicate In the box:

Ca- Copy without enclosures

E - Copy with enclosures

EN" = No copy

IOFFICE

TECH

CONTACT

S

C:EELB

C:PECB

D:DRPM

NAME

APa1*

JCalvo*

AChaffee

TMartin

TKoshy A

DSkeen*

DATE

1046997

04/

/97

04/

/97

104/ /97

OFFICIAL RECORD WPY7

I 1W7-xx

March xx, 1997 safety related power supply and had been out for an extended period during the loss of

offsite power. This extended loss of auxiliary power caused the oil temperature to drop

below the minimum temperature required for DG operation.

Discussion

The Millstone licensee reviewed the design and operation of the AAC power source at

Millstone Unit 3 and determined that the AAC power source required modification to

assure availability of the SBO DG for no less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (the probable time needed to

restore offsite power) following a postulated LOOP event.

The Pilgrim licensee discovered that the SBO DG was susceptible to a failure to start as a

result of low oil temperature if power was lost to the lubricating oil keep-warm system for

an extended period.

The licensee is considering enhanced monitoring of SBO DG

auxiliaries, procedural changes or modifications to SBO DG start logic.

The SBO DG capability to start on demand depends on the availability of the necessary

support systems to fulfill their required function. The SBO DG support systems may

require varying combinations of dc or ac power for varying periods to maintain operational

readiness. Prompt operator actions to conserve battery capacity, support system power

supply modifications, use of special procedures, or start logic modifications may be

necessary to preserve the operational readiness of the SBO DG under challenging

environmental conditions. The staff is evaluating these events and the consequential need

for additional generic communications.

This information notice requires no specific action or written response. If you have any

questions about the information in this notice, please contact one of the technical contacts

listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project

manager.

Thomas T. Martin, Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical Contacts: A. Pal, NRR

Thomas Koshy

David Skeen

(301) 415-2760

(301) 415-1176 (301) 415-1174 E-mail:ANP@NRC.GOV TXK@NRC.GOV DLS@NRC.GOV

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\\TXK\\SBO.3 To receive a copy of this document, Indicate in the box: 'C' - Copy without enclosures

'E" - Copy with enclosures

N - No copy

OFFICE

TECH

CONTACT

S I

IC:EELB

TI

C:PECB

I

ID:DRPM

I

NAME

APa1*

JCalvo*

AChaffee

TMartin

7Koshy

oats

DSkeen*_

DATE

04/? /97

04/

/97

04/

/97

04/

/97 OFFICIAL RECORD COPY