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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                                NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                                REGION II
REGION II  
                                SAM NUNN ATLANTA FEDERAL CENTER
SAM NUNN ATLANTA FEDERAL CENTER
                                  61 FORSYTH STREET, SW, SUITE 23T85
61 FORSYTH STREET, SW, SUITE 23T85  
                                      ATLANTA, GEORGIA 30303-8931
ATLANTA, GEORGIA 30303-8931  
                                            October 30, 2009
Mr. Christopher L. Burton
October 30, 2009  
Vice President
Carolina Power & Light Company
Shearon Harris Nuclear Plant
P.O. Box 165, Mail Zone 1
Mr. Christopher L. Burton  
New Hill, NC 27562-0165
Vice President  
SUBJECT:         SHEARON HARRIS NUCLEAR POWER PLANT - NRC PROBLEM
Carolina Power & Light Company  
                IDENTIFICATION AND RESOLUTION INSPECTION
Shearon Harris Nuclear Plant  
                REPORT 05000400/2009006
P.O. Box 165, Mail Zone 1  
Dear Mr. Burton:
New Hill, NC 27562-0165  
On October 2, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection
at your Shearon Harris reactor facility. The enclosed report documents the inspection findings,
SUBJECT:  
which were discussed on October 2, 2009, and October 26, 2009, with you and other members
SHEARON HARRIS NUCLEAR POWER PLANT - NRC PROBLEM  
of your staff.
IDENTIFICATION AND RESOLUTION INSPECTION  
The inspection was an examination of activities conducted under your license as they relate to
REPORT 05000400/2009006  
the identification and resolution of problems, compliance with the Commissions rules and
regulations, and with the conditions of your operating license. Within these areas, the
Dear Mr. Burton:  
inspection involved examination of selected procedures and representative records,
observations of plant equipment and activities, and interviews with personnel.
On October 2, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection  
On the basis of the samples selected for review, the team concluded that in general, problems
at your Shearon Harris reactor facility. The enclosed report documents the inspection findings,  
were properly identified, evaluated, and resolved within the problem identification and resolution
which were discussed on October 2, 2009, and October 26, 2009, with you and other members  
program. However, during the inspection, some examples of minor issues were identified in the
of your staff.  
areas of identification of issues, prioritization and evaluation of issues, and effectiveness of
corrective actions. This report documents two NRC identified findings that were evaluated
The inspection was an examination of activities conducted under your license as they relate to  
under the significance determination process as having very low safety significance (Green).
the identification and resolution of problems, compliance with the Commissions rules and  
These issues were determined to involve violations of NRC requirements. However, because of
regulations, and with the conditions of your operating license. Within these areas, the  
their very low safety significance and because they were entered into your corrective action
inspection involved examination of selected procedures and representative records,  
program, the NRC is treating these findings as non-cited violations consistent with
observations of plant equipment and activities, and interviews with personnel.  
Section VI.A.1 of the NRC Enforcement Policy. If you wish to contest these non-cited violations,
you should provide a response within 30 days of the date of this inspection report, with the basis
On the basis of the samples selected for review, the team concluded that in general, problems  
for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk,
were properly identified, evaluated, and resolved within the problem identification and resolution  
Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director,
program. However, during the inspection, some examples of minor issues were identified in the  
Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC
areas of identification of issues, prioritization and evaluation of issues, and effectiveness of  
20555-0001; and the NRC Senior Resident Inspector at the Shearon Harris Nuclear Plant.
corrective actions. This report documents two NRC identified findings that were evaluated  
under the significance determination process as having very low safety significance (Green).
These issues were determined to involve violations of NRC requirements. However, because of  
their very low safety significance and because they were entered into your corrective action  
program, the NRC is treating these findings as non-cited violations consistent with  
Section VI.A.1 of the NRC Enforcement Policy. If you wish to contest these non-cited violations,  
you should provide a response within 30 days of the date of this inspection report, with the basis  
for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk,  
Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director,  
Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC  
20555-0001; and the NRC Senior Resident Inspector at the Shearon Harris Nuclear Plant.  


CP&L                                         2
CP&L  
In addition, if you disagree with the characterization of any finding in this report, you should
2  
provide a response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Shearon Harris Power Plant. The information you provide will be considered in accordance with
In addition, if you disagree with the characterization of any finding in this report, you should  
Inspection Manual Chapter 0305.
provide a response within 30 days of the date of this inspection report, with the basis for your  
In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the  
enclosure, and your response (if any), will be available electronically for public inspection in the
Shearon Harris Power Plant. The information you provide will be considered in accordance with  
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
Inspection Manual Chapter 0305.  
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its  
                                              Sincerely,
enclosure, and your response (if any), will be available electronically for public inspection in the  
                                              /RA/
NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
                                              Daniel Merzke, Acting Chief
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at  
                                              Reactor Projects Branch 7
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
                                              Division of Reactor Projects
Docket Nos. 50-400
License Nos. DPR-63
Enclosure:       Inspection Report 05000400/2009006
                w/Attachment: Supplemental Information
cc w/encl. (See page 3)
Sincerely,  
/RA/  
Daniel Merzke, Acting Chief  
Reactor Projects Branch 7  
Division of Reactor Projects  
Docket Nos.  
50-400  
License Nos. DPR-63  
Enclosure:  
Inspection Report 05000400/2009006  
w/Attachment: Supplemental Information  
cc w/encl. (See page 3)  


  CP&L                                         2
  CP&L  
In addition, if you disagree with the characterization of any finding in this report, you should
2  
provide a response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
Shearon Harris Power Plant. The information you provide will be considered in accordance with
In addition, if you disagree with the characterization of any finding in this report, you should  
Inspection Manual Chapter 0305.
provide a response within 30 days of the date of this inspection report, with the basis for your  
In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the  
enclosure, and your response (if any), will be available electronically for public inspection in the
Shearon Harris Power Plant. The information you provide will be considered in accordance with  
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
Inspection Manual Chapter 0305.  
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its  
                                              Sincerely,
enclosure, and your response (if any), will be available electronically for public inspection in the  
                                              /RA/
NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
                                              Daniel Merzke, Acting Chief
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at  
                                              Reactor Projects Branch 7
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
                                              Division of Reactor Projects
Docket Nos. 50-400
License Nos. DPR-63
Enclosure:       Inspection Report 05000400/2009006
                w/Attachment: Supplemental Information
cc w/encl. (See page 3)
  SUNSI Rev Compl.       ; Yes     No   ADAMS         ; Yes No         Reviewer Initials
  Publicly Avail         ; Yes     No   Sensitive       Yes ; No       Sens. Type Initials
Sincerely,  
  RIV:DRP           RII:DRP         RII:DRP         RII:DRS           RII:DRP
  MCatts           PLessard         PNiebaum         RTaylor           EStamm
  MPS4 by email     PBL1 by email   PKN by email     RCT1 by email     EJS2
  10/29/09         10/29/09         10/29/09         10/29/09         10/30/09
  RII:DRP           RII:DRP
  DMerzke           RMusser
  DXM2             RAM
  10/30/09         10/30/09
/RA/  
OFFICIAL RECORD COPY    DOCUMENT NAME: S:\DRP\RPB7\PI&R\PI&R\InspectionReports\Harris PIR Inspection
Report 2009006 rev 7.doc                   T=Telephone          E=E-mail        F=Fax
Daniel Merzke, Acting Chief  
Reactor Projects Branch 7  
Division of Reactor Projects  
Docket Nos.  
50-400  
License Nos. DPR-63  
Enclosure:  
Inspection Report 05000400/2009006  
w/Attachment: Supplemental Information  
cc w/encl. (See page 3)  
SUNSI Rev Compl.  
; Yes No  
ADAMS  
; Yes No  
Reviewer Initials  
Publicly Avail  
; Yes No  
Sensitive  
Yes ; No  
Sens. Type Initials  
   
RIV:DRP  
RII:DRP  
RII:DRP  
RII:DRS  
RII:DRP  
   
MCatts  
PLessard  
PNiebaum  
RTaylor  
EStamm  
   
MPS4 by email PBL1 by email PKN by email  
RCT1 by email EJS2  
   
10/29/09  
10/29/09  
10/29/09  
10/29/09  
10/30/09  
   
RII:DRP  
RII:DRP  
   
DMerzke  
RMusser  
   
DXM2  
RAM  
   
10/30/09  
10/30/09  
OFFICIAL RECORD COPY    DOCUMENT NAME: S:\\DRP\\RPB7\\PI&R\\PI&R\\InspectionReports\\Harris PIR Inspection  
Report 2009006 rev 7.doc
 
        T=Telephone          E=E-mail        F=Fax


CP&L                                 3
CP&L  
cc w/encl:
3  
Brian C. McCabe                       Chairman
Manager, Nuclear Regulatory Affairs   North Carolina Utilities Commission
Progress Energy Carolinas, Inc.       Electronic Mail Distribution
cc w/encl:  
Electronic Mail Distribution
Brian C. McCabe  
                                      Beverly O. Hall
Manager, Nuclear Regulatory Affairs  
R. J. Duncan, II                      Chief, Radiation Protection Section
Progress Energy Carolinas, Inc.
Vice President                        Department of Environmental Health
Electronic Mail Distribution
Nuclear Operations                    N.C. Department of Environmental
Carolina Power & Light Company        Commerce & Natural Resources
R. J. Duncan, II
Electronic Mail Distribution           Electronic Mail Distribution
Vice President
Greg Kilpatrick                        Public Service Commission
Nuclear Operations
Training Manager                      State of South Carolina
Carolina Power & Light Company
Shearon Harris Nuclear Power Plant    P.O. Box 11649
Electronic Mail Distribution
Progress Energy Carolinas, Inc.        Columbia, SC 29211
Electronic Mail Distribution
Greg Kilpatrick
                                      Robert P. Gruber
Training Manager
John Warner                            Executive Director
Shearon Harris Nuclear Power Plant
Manager                                Public Staff - NCUC
Progress Energy Carolinas, Inc.
Support Services                      4326 Mail Service Center
Electronic Mail Distribution
Progress Energy Carolinas, Inc.        Raleigh, NC 27699-4326
Electronic Mail Distribution
John Warner
                                      Herb Council
Manager
David H. Corlett                      Chair
Support Services
Supervisor                            Board of County Commissioners of Wake
Progress Energy Carolinas, Inc.  
Licensing/Regulatory Programs          County
Electronic Mail Distribution
Progress Energy                        P.O. Box 550
Electronic Mail Distribution          Raleigh, NC 27602
David H. Corlett
David T. Conley                        Tommy Emerson
Supervisor
Associate General Counsel              Chair
Licensing/Regulatory Programs
Legal Dept.                            Board of County Commissioners of
Progress Energy
Progress Energy Service Company, LLC  Chatham County
Electronic Mail Distribution  
Electronic Mail Distribution          186 Emerson Road
                                      Siler City, NC 27344
David T. Conley
Christos Kamilaris
Associate General Counsel
Director                              Kelvin Henderson
Legal Dept.
Fleet Support Services                Plant General Manager
Progress Energy Service Company, LLC
Carolina Power & Light Company        Carolina Power and Light Company
Electronic Mail Distribution  
Electronic Mail Distribution          Shearon Harris Nuclear Power Plant
                                      Electronic Mail Distribution
Christos Kamilaris
John H. O'Neill, Jr.
Director
Shaw, Pittman, Potts & Trowbridge      cc w/encl. (continued page 4)
Fleet Support Services
2300 N. Street, NW
Carolina Power & Light Company
Washington, DC 20037-1128
Electronic Mail Distribution
John H. O'Neill, Jr.
Shaw, Pittman, Potts & Trowbridge
2300 N. Street, NW
Washington, DC 20037-1128
Chairman
North Carolina Utilities Commission
Electronic Mail Distribution
Beverly O. Hall  
Chief, Radiation Protection Section  
Department of Environmental Health  
N.C. Department of Environmental  
Commerce & Natural Resources  
Electronic Mail Distribution  
Public Service Commission  
State of South Carolina  
P.O. Box 11649  
Columbia, SC 29211  
Robert P. Gruber  
Executive Director  
Public Staff - NCUC  
4326 Mail Service Center  
Raleigh, NC 27699-4326  
Herb Council  
Chair  
Board of County Commissioners of Wake  
County  
P.O. Box 550  
Raleigh, NC 27602  
Tommy Emerson  
Chair  
Board of County Commissioners of  
Chatham County  
186 Emerson Road  
Siler City, NC 27344  
Kelvin Henderson  
Plant General Manager  
Carolina Power and Light Company  
Shearon Harris Nuclear Power Plant  
Electronic Mail Distribution  
cc w/encl. (continued page 4)  


CP&L                               4
CP&L  
cc w/encl. (continued)
4  
Senior Resident Inspector
Carolina Power and Light Company
Shearon Harris Nuclear Power Plant
cc w/encl. (continued)  
U.S. NRC
Senior Resident Inspector  
5421 Shearon Harris Rd
Carolina Power and Light Company  
New Hill, NC 27562-9998
Shearon Harris Nuclear Power Plant  
U.S. NRC  
5421 Shearon Harris Rd  
New Hill, NC 27562-9998  
                                                                     


CP&L                                       5
CP&L  
Letter to Christopher L. Burton from Daniel Merzke dated October 30, 2009.
5  
SUBJECT:       SHEARON HARRIS NUCLEAR POWER PLANT - NRC PROBLEM
                IDENTIFICATION AND RESOLUTION INSPECTION REPORT
                05000400/2009006
Letter to Christopher L. Burton from Daniel Merzke dated October 30, 2009.  
Distribution w/encl:
C. Evans, RII EICS
SUBJECT:  
L. Slack, RII EICS
SHEARON HARRIS NUCLEAR POWER PLANT - NRC PROBLEM  
OE Mail
IDENTIFICATION AND RESOLUTION INSPECTION REPORT  
RIDSNRRDIRS
05000400/2009006  
PUBLIC
RidsNrrPMShearonHarris Resource
Distribution w/encl:  
C. Evans, RII EICS  
L. Slack, RII EICS  
OE Mail  
RIDSNRRDIRS  
PUBLIC  
RidsNrrPMShearonHarris Resource  


          U.S. NUCLEAR REGULATORY COMMISSION
                          REGION II
Enclosure
Docket Nos.:       50-400
U.S. NUCLEAR REGULATORY COMMISSION  
License Nos.:       DPR-63
Report No:         05000400/2009006
REGION II  
Licensee:           Carolina Power and Light Company (CP&L)
Facility:           Shearon Harris Nuclear Power Plant, Unit 1
Location:           5413 Shearon Harris Road
                    New Hill, NC 27562
Docket Nos.:
Dates:             September 14 - 18, 2009
50-400  
                    September 28 - October 2, 2009
Inspectors:         M. Catts, Resident Inspector, Palo Verde, Team Leader
                    P. Lessard, Resident Inspector, Harris
License Nos.:
                    P. Niebaum, Resident Inspector, Hatch
DPR-63  
                    R. Taylor, Senior Project Inspector
                    E. Stamm, Project Engineer
Approved by:       Daniel Merzke, Acting Chief
Report No:  
                    Reactor Projects Branch 7
                    Division of Reactor Projects
05000400/2009006  
                                                                  Enclosure
Licensee:  
Carolina Power and Light Company (CP&L)  
Facility:  
Shearon Harris Nuclear Power Plant, Unit 1  
Location:  
5413 Shearon Harris Road  
New Hill, NC 27562  
Dates:
September 14 - 18, 2009  
September 28 - October 2, 2009  
Inspectors:  
M. Catts, Resident Inspector, Palo Verde, Team Leader  
P. Lessard, Resident Inspector, Harris  
P. Niebaum, Resident Inspector, Hatch
R. Taylor, Senior Project Inspector  
E. Stamm, Project Engineer  
Approved by:
Daniel Merzke, Acting Chief  
Reactor Projects Branch 7  
Division of Reactor Projects  


                                    SUMMARY OF FINDINGS
IR 05000400/2009006; 09/14/2009 - 10/02/2009; Shearon Harris Nuclear Power
Plant, Unit 1; biennial inspection of the identification and resolution of problems.
Enclosure
The inspection was conducted by a senior project inspector, three resident inspectors, and a
SUMMARY OF FINDINGS  
project engineer. Two Green findings of very low safety significance were identified during the
inspection. The significance of most findings is indicated by their color (Green, White, Yellow,
or Red) using Inspection Manual Chapter 0609, "Significance Determination Process." The
IR 05000400/2009006; 09/14/2009 - 10/02/2009; Shearon Harris Nuclear Power  
cross-cutting aspects were determined using Inspection Manual Chapter 0305, "Operating
Plant, Unit 1; biennial inspection of the identification and resolution of problems.  
Reactor Assessment Program." Findings for which the significance determination process does
not apply may be Green or be assigned a severity level after NRC management's review. The
The inspection was conducted by a senior project inspector, three resident inspectors, and a  
NRCs program for overseeing the safe operation of commercial nuclear power reactors is
project engineer. Two Green findings of very low safety significance were identified during the  
described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
inspection. The significance of most findings is indicated by their color (Green, White, Yellow,  
Identification and Resolution of Problems
or Red) using Inspection Manual Chapter 0609, "Significance Determination Process." The  
The inspection team concluded that, in general, problems were adequately identified, prioritized,
cross-cutting aspects were determined using Inspection Manual Chapter 0305, "Operating  
and evaluated; and effective corrective actions were implemented. Site management was
Reactor Assessment Program." Findings for which the significance determination process does  
actively involved in the corrective action program and focused appropriate attention on
not apply may be Green or be assigned a severity level after NRC management's review. The  
significant plant issues. The team found that employees were encouraged by management to
NRCs program for overseeing the safe operation of commercial nuclear power reactors is  
initiate corrective action documents to address plant issues.
described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.  
The licensee generally had an adequate threshold for identifying and correcting problems, as
evidenced by the relatively few deficiencies identified by the NRC that had not been previously
Identification and Resolution of Problems  
identified by the licensee during the review period. Action requests normally provided complete
and accurate characterization of the problem. However, the team identified a minor violation
The inspection team concluded that, in general, problems were adequately identified, prioritized,  
and seven minor issues during plant walkdowns and document reviews where problems were
and evaluated; and effective corrective actions were implemented. Site management was  
not identified and entered into the corrective action program by the licensee.
actively involved in the corrective action program and focused appropriate attention on  
Generally, prioritization and evaluation of issues were adequate, consistent with the licensees
significant plant issues. The team found that employees were encouraged by management to  
corrective action program guidance. Formal root cause evaluations for significant problems
initiate corrective action documents to address plant issues.  
were adequate, and corrective actions specified for problems addressed the cause of the
problems. The age and extensions for completing evaluations were closely monitored by plant
The licensee generally had an adequate threshold for identifying and correcting problems, as  
management, both for high priority nuclear condition reports, as well as for adverse conditions
evidenced by the relatively few deficiencies identified by the NRC that had not been previously  
of lower priority. Also, the technical adequacy and depth of evaluations (e.g., root cause
identified by the licensee during the review period. Action requests normally provided complete  
investigations) were typically adequate. However, the team identified one unresolved item and
and accurate characterization of the problem. However, the team identified a minor violation  
two minor issues associated with prioritization and evaluation of issues.
and seven minor issues during plant walkdowns and document reviews where problems were  
Corrective actions were generally timely, commensurate with the safety significance of the
not identified and entered into the corrective action program by the licensee.  
issues, and effective, in that conditions adverse to quality were corrected in accordance with the
licensee CAP procedures. For the significant conditions adverse to quality that were reviewed,
Generally, prioritization and evaluation of issues were adequate, consistent with the licensees  
generally the corrective actions directly addressed the cause and effectively prevented
corrective action program guidance. Formal root cause evaluations for significant problems  
recurrence, as evidenced by a review of performance indicators, nuclear condition reports, and
were adequate, and corrective actions specified for problems addressed the cause of the  
discussions with licensee staff that demonstrated that the significant conditions adverse to
problems. The age and extensions for completing evaluations were closely monitored by plant  
quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence
management, both for high priority nuclear condition reports, as well as for adverse conditions  
were scheduled consistent with licensee procedures. However, during the review of nuclear
of lower priority. Also, the technical adequacy and depth of evaluations (e.g., root cause  
                                                                                        Enclosure
investigations) were typically adequate. However, the team identified one unresolved item and  
two minor issues associated with prioritization and evaluation of issues.  
Corrective actions were generally timely, commensurate with the safety significance of the  
issues, and effective, in that conditions adverse to quality were corrected in accordance with the  
licensee CAP procedures. For the significant conditions adverse to quality that were reviewed,  
generally the corrective actions directly addressed the cause and effectively prevented  
recurrence, as evidenced by a review of performance indicators, nuclear condition reports, and  
discussions with licensee staff that demonstrated that the significant conditions adverse to  
quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence  
were scheduled consistent with licensee procedures. However, during the review of nuclear


                                                    3
3  
condition reports, the team identified two violations of NRC requirements and an additional
minor issue regarding adequacy and timeliness of corrective actions.
Enclosure
The operating experience program was effective in screening operating experience for
condition reports, the team identified two violations of NRC requirements and an additional  
applicability to the plant, entering items determined to be applicable into the corrective action
minor issue regarding adequacy and timeliness of corrective actions.
program, and taking adequate corrective actions to address the issues. External and internal
operating experience were adequately utilized and considered as part of formal root cause
The operating experience program was effective in screening operating experience for  
evaluations for supporting the development of lessons learned and corrective actions.
applicability to the plant, entering items determined to be applicable into the corrective action  
The licensees audits and self-assessments were critical and effective in identifying issues and
program, and taking adequate corrective actions to address the issues. External and internal  
entering them into the corrective action program. These audits and assessments identified
operating experience were adequately utilized and considered as part of formal root cause  
issues similar to those identified by the NRC with respect to the effectiveness of the corrective
evaluations for supporting the development of lessons learned and corrective actions.  
action program.
Based on general discussions with licensee employees during the inspection, targeted
The licensees audits and self-assessments were critical and effective in identifying issues and  
interviews with plant personnel, and reviews of selected employee concerns records, the team
entering them into the corrective action program. These audits and assessments identified  
determined that personnel at the site felt free to raise safety concerns to management and use
issues similar to those identified by the NRC with respect to the effectiveness of the corrective  
the corrective action program as well as the employee concerns program to resolve those
action program.  
concerns.
A.     NRC Identified Findings
Based on general discussions with licensee employees during the inspection, targeted  
        Cornerstone: Barrier Integrity
interviews with plant personnel, and reviews of selected employee concerns records, the team  
        *       Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,
determined that personnel at the site felt free to raise safety concerns to management and use  
                Criterion XVI, "Corrective Action," for the licensees failure to identify the cause
the corrective action program as well as the employee concerns program to resolve those  
                and take corrective actions to preclude repetition of a significant condition
concerns.  
                adverse to quality for both containment spray additive system eductors being
                outside of the technical specification flow band. Specifically, between July 2009
A.  
                and the present, the violation occurred when Eductor A was found three times
NRC Identified Findings
                and Eductor B was found once outside of the Technical Specification 3.6.2.2 flow
                band. This issue was previously identified as a significant condition adverse to
Cornerstone: Barrier Integrity  
                quality in January 2008, but the corrective actions taken failed to preclude
                repetition. The licensee entered this issue into the corrective action program as
*  
                nuclear condition report 356873. The licensee took immediate corrective actions
Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,  
                to throttle the eductor flow to within the band, and is developing corrective
Criterion XVI, "Corrective Action," for the licensees failure to identify the cause  
                actions to preclude repetition.
and take corrective actions to preclude repetition of a significant condition  
                The finding is more than minor because it is associated with the design control
adverse to quality for both containment spray additive system eductors being  
                attribute of the Barrier Integrity Cornerstone and affects the cornerstone objective
outside of the technical specification flow band. Specifically, between July 2009  
                of providing reasonable assurance that physical design barriers, such as the
and the present, the violation occurred when Eductor A was found three times  
                iodine scrubbing capability of the containment spray additive system eductors,
and Eductor B was found once outside of the Technical Specification 3.6.2.2 flow  
                will protect the public from radionuclide releases caused by accidents or events.
band. This issue was previously identified as a significant condition adverse to  
                Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and
quality in January 2008, but the corrective actions taken failed to preclude  
                Characterization of Findings," the finding was determined to have a very low
repetition. The licensee entered this issue into the corrective action program as  
                safety significance because it did not represent a degradation of the radiological
nuclear condition report 356873. The licensee took immediate corrective actions  
                barrier function provided for the control room, auxiliary building, or spent fuel
to throttle the eductor flow to within the band, and is developing corrective  
                pool; the finding did not represent a degradation of the barrier function of the
actions to preclude repetition.  
                                                                                              Enclosure
The finding is more than minor because it is associated with the design control  
attribute of the Barrier Integrity Cornerstone and affects the cornerstone objective  
of providing reasonable assurance that physical design barriers, such as the  
iodine scrubbing capability of the containment spray additive system eductors,  
will protect the public from radionuclide releases caused by accidents or events.
Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and  
Characterization of Findings," the finding was determined to have a very low  
safety significance because it did not represent a degradation of the radiological  
barrier function provided for the control room, auxiliary building, or spent fuel  
pool; the finding did not represent a degradation of the barrier function of the  


                                              4
4  
          control room against smoke or a toxic atmosphere; the finding did not represent
          an actual open pathway in the physical integrity of reactor containment; and the
Enclosure
          finding did not involve an actual reduction in function of the hydrogen igniters in
control room against smoke or a toxic atmosphere; the finding did not represent  
          the reactor containment. The finding had a cross-cutting aspect in the area of
an actual open pathway in the physical integrity of reactor containment; and the  
          problem identification and resolution associated with the corrective action
finding did not involve an actual reduction in function of the hydrogen igniters in  
          program because the licensee did not thoroughly evaluate problems such that
the reactor containment. The finding had a cross-cutting aspect in the area of  
          the resolutions address causes and extent of conditions, as necessary, and for
problem identification and resolution associated with the corrective action  
          significant problems, conduct effectiveness reviews of corrective actions to
program because the licensee did not thoroughly evaluate problems such that  
          ensure that the problems are resolved (P.1(c)) (Section 4OA2.a(3)(i)).
the resolutions address causes and extent of conditions, as necessary, and for  
  *     Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,
significant problems, conduct effectiveness reviews of corrective actions to  
          Criterion XVI, "Corrective Action," for the licensees failure to correct a condition
ensure that the problems are resolved (P.1(c)) (Section 4OA2.a(3)(i)).  
          adverse to quality in a timely manner. Specifically, between May 27, 1997 and
          September 29, 2007, Main Steam Isolation Valve 82 close stroke time exhibited
*  
          a condition adverse to quality for a trend degrading towards the technical
Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,  
          specification limit, without sufficient corrective actions to prevent failure. This
Criterion XVI, "Corrective Action," for the licensees failure to correct a condition  
          resulted in Main Steam Isolation Valve 82 exceeding the five-second stroke time
adverse to quality in a timely manner. Specifically, between May 27, 1997 and  
          limit required in Technical Specification 3.7.1.5. The licensee entered this issue
September 29, 2007, Main Steam Isolation Valve 82 close stroke time exhibited  
          into the corrective action program as nuclear condition report 358464.
a condition adverse to quality for a trend degrading towards the technical  
          This finding is more than minor because it is associated with the containment
specification limit, without sufficient corrective actions to prevent failure. This  
          barrier performance attribute of the Barrier Integrity Cornerstone and affects the
resulted in Main Steam Isolation Valve 82 exceeding the five-second stroke time  
          cornerstone objective of providing reasonable assurance that physical design
limit required in Technical Specification 3.7.1.5. The licensee entered this issue  
          barriers, such as the main steam isolation valve radiological release barrier
into the corrective action program as nuclear condition report 358464.  
          required for a steam generator tube rupture, protect the public from radionuclide
          releases caused by accidents or events. Using Manual Chapter 0609.04, "Phase
This finding is more than minor because it is associated with the containment  
          1 - Initial Screening and Characterization of Findings," the finding was
barrier performance attribute of the Barrier Integrity Cornerstone and affects the  
          determined to have a very low safety significance because it did not represent a
cornerstone objective of providing reasonable assurance that physical design  
          degradation of the radiological barrier function provided for the control room,
barriers, such as the main steam isolation valve radiological release barrier  
          auxiliary building, or spent fuel pool; the finding did not represent a degradation
required for a steam generator tube rupture, protect the public from radionuclide  
          of the barrier function of the control room against smoke or a toxic atmosphere;
releases caused by accidents or events. Using Manual Chapter 0609.04, "Phase  
          the finding did not represent an actual open pathway in the physical integrity of
1 - Initial Screening and Characterization of Findings," the finding was  
          reactor containment; and the finding did not involve an actual reduction in
determined to have a very low safety significance because it did not represent a  
          function of the hydrogen igniters in the reactor containment. This finding had a
degradation of the radiological barrier function provided for the control room,  
          cross-cutting aspect in the area of human performance associated with decision-
auxiliary building, or spent fuel pool; the finding did not represent a degradation  
          making because the licensee did not use conservative assumptions so that
of the barrier function of the control room against smoke or a toxic atmosphere;  
          safety-significant decisions were verified to validate underlying assumptions and
the finding did not represent an actual open pathway in the physical integrity of  
          identify unintended consequences (H.1.(b)) (Section 4OA2.a(3)(ii)).
reactor containment; and the finding did not involve an actual reduction in  
B. Licensee Identified Violations
function of the hydrogen igniters in the reactor containment. This finding had a  
  None
cross-cutting aspect in the area of human performance associated with decision-
                                                                                        Enclosure
making because the licensee did not use conservative assumptions so that  
safety-significant decisions were verified to validate underlying assumptions and  
identify unintended consequences (H.1.(b)) (Section 4OA2.a(3)(ii)).  
B.  
Licensee Identified Violations  
None  


                                    REPORT DETAILS
4.   OTHER ACTIVITIES
Enclosure
4OA2 Problem Identification and Resolution
REPORT DETAILS  
  a. Assessment of the Corrective Action Program
  (1) Inspection Scope
    The inspectors reviewed the licensees corrective action program (CAP) procedures
4.  
    which described the administrative process for initiating and resolving problems primarily
OTHER ACTIVITIES  
    through the use of action requests (ARs), which were then processed into the CAP as
    nuclear condition reports (NCRs). The team selected and reviewed a sample of NCRs
 
    that had been issued between August 2007 and August 2009. This period of time was
4OA2 Problem Identification and Resolution  
    purposefully chosen to follow the last Biennial Problem Identification and Resolution
   
    (PI&R) inspection conducted in August 2007. This review was performed to verify that
    problems were being properly identified, appropriately characterized, and entered into
  a.  
    the CAP for resolution. Where possible, the team independently verified that the
Assessment of the Corrective Action Program  
    corrective actions were implemented as intended.
   
    Within the time frame described above, the team selected NCRs from principally four
  (1)  
    specific areas of interest. The first inspection area consisted of a detailed review of
Inspection Scope  
    selected NCRs associated with four risk-significant systems: emergency AC power (non-
    emergency diesel generator (EDG)), essential services chilled water, containment
The inspectors reviewed the licensees corrective action program (CAP) procedures  
    isolation Target Rock valves, and low head safety injection (LHSI) / residual heat
which described the administrative process for initiating and resolving problems primarily  
    removal (RHR) system. The team conducted plant walkdowns of equipment associated
through the use of action requests (ARs), which were then processed into the CAP as  
    with the selected systems and other plant areas to assess the material condition and to
nuclear condition reports (NCRs). The team selected and reviewed a sample of NCRs  
    look for any deficiencies that had not been previously entered into the CAP. The team
that had been issued between August 2007 and August 2009. This period of time was  
    reviewed NCRs, maintenance history, completed work orders (WOs) for the systems,
purposefully chosen to follow the last Biennial Problem Identification and Resolution  
    and reviewed associated system health reports. These reviews were performed to verify
(PI&R) inspection conducted in August 2007. This review was performed to verify that  
    that problems were being properly identified, appropriately characterized, and entered
problems were being properly identified, appropriately characterized, and entered into  
    into the CAP for resolution. Items reviewed generally covered a two-year period of time;
the CAP for resolution. Where possible, the team independently verified that the  
    however, in accordance with the inspection procedure, the team performed a five-year
corrective actions were implemented as intended.  
    review of age-dependent issues for containment isolation Target Rock valves and
    LHSI/RHR.
Within the time frame described above, the team selected NCRs from principally four  
    The second inspection area consisted of a detailed review of a representative number of
specific areas of interest. The first inspection area consisted of a detailed review of  
    NCRs that were assigned to the major plant departments, including operations,
selected NCRs associated with four risk-significant systems: emergency AC power (non-  
    maintenance, engineering, health physics, chemistry, emergency preparedness, and
emergency diesel generator (EDG)), essential services chilled water, containment  
    security. This selection was performed to ensure that samples were reviewed across all
isolation Target Rock valves, and low head safety injection (LHSI) / residual heat  
    cornerstones of safety identified in the NRCs Reactor Oversight Process (ROP). These
removal (RHR) system. The team conducted plant walkdowns of equipment associated  
    NCRs were reviewed to assess each departments threshold for identifying and
with the selected systems and other plant areas to assess the material condition and to  
    documenting plant problems, thoroughness of evaluations, and adequacy of corrective
look for any deficiencies that had not been previously entered into the CAP. The team  
    actions. The team also attended meetings where NCRs were screened for significance
reviewed NCRs, maintenance history, completed work orders (WOs) for the systems,  
                                                                                        Enclosure
and reviewed associated system health reports. These reviews were performed to verify  
that problems were being properly identified, appropriately characterized, and entered  
into the CAP for resolution. Items reviewed generally covered a two-year period of time;  
however, in accordance with the inspection procedure, the team performed a five-year  
review of age-dependent issues for containment isolation Target Rock valves and  
LHSI/RHR.  
The second inspection area consisted of a detailed review of a representative number of  
NCRs that were assigned to the major plant departments, including operations,  
maintenance, engineering, health physics, chemistry, emergency preparedness, and  
security. This selection was performed to ensure that samples were reviewed across all  
cornerstones of safety identified in the NRCs Reactor Oversight Process (ROP). These  
NCRs were reviewed to assess each departments threshold for identifying and  
documenting plant problems, thoroughness of evaluations, and adequacy of corrective  
actions. The team also attended meetings where NCRs were screened for significance  


                                              6
    to determine whether the licensee was identifying, accurately characterizing, and
    entering problems into the CAP at an appropriate threshold.
    For the third inspection area, the team selected a sample of NRC issued non-cited
Enclosure
    violations and findings, licensee identified violations, and Licensee Event Reports
6
    (LERs), to verify the effectiveness of the licensees CAP implementation regarding NRC
to determine whether the licensee was identifying, accurately characterizing, and  
    inspection findings and reportable events issued since the previous 2007 PI&R
entering problems into the CAP at an appropriate threshold.  
    inspection.
    The fourth inspection area covered the review of NCRs associated with selected issues
For the third inspection area, the team selected a sample of NRC issued non-cited  
    of interest, specifically maintenance rule functional failures, non-conforming/degraded
violations and findings, licensee identified violations, and Licensee Event Reports  
    conditions, and radiation monitors performance issues. The team reviewed the NCRs to
(LERs), to verify the effectiveness of the licensees CAP implementation regarding NRC  
    verify that problems were identified, evaluated, and resolved in accordance with the
inspection findings and reportable events issued since the previous 2007 PI&R  
    licensees procedures and applicable NRC Regulations.
inspection.  
    Among the four areas mentioned above, the team conducted a detailed review of
    selected root-cause and apparent-cause evaluations of the problems identified. The
The fourth inspection area covered the review of NCRs associated with selected issues  
    team reviewed these evaluations against the descriptions of the problem described in
of interest, specifically maintenance rule functional failures, non-conforming/degraded  
    the NCRs and the guidance in licensee Procedure CAP-NGGC-0205, "Significant
conditions, and radiation monitors performance issues. The team reviewed the NCRs to  
    Adverse Condition Investigations and Adverse Condition Investigations-Increased
verify that problems were identified, evaluated, and resolved in accordance with the  
    Rigor." The team assessed if the licensee had adequately determined the cause(s) of
licensees procedures and applicable NRC Regulations.  
    identified problems, and had adequately addressed operability, reportability, common
    cause, generic concerns, extent-of-condition, and extent-of-cause. The review also
Among the four areas mentioned above, the team conducted a detailed review of  
    assessed if the licensee had appropriately identified and prioritized corrective actions to
selected root-cause and apparent-cause evaluations of the problems identified. The  
    prevent recurrence.
team reviewed these evaluations against the descriptions of the problem described in  
    Additionally, the team performed control room walkdowns to assess the main control
the NCRs and the guidance in licensee Procedure CAP-NGGC-0205, "Significant  
    room (MCR) deficiency list and to ascertain if deficiencies were entered into the CAP.
Adverse Condition Investigations and Adverse Condition Investigations-Increased  
    Operator workarounds and operator burden screenings were reviewed, and the team
Rigor." The team assessed if the licensee had adequately determined the cause(s) of  
    verified compensatory measures for deficient equipment which were being implemented
identified problems, and had adequately addressed operability, reportability, common  
    in the field.
cause, generic concerns, extent-of-condition, and extent-of-cause. The review also  
    Finally, the team reviewed site trend reports, to determine if the licensee effectively
assessed if the licensee had appropriately identified and prioritized corrective actions to  
    trended identified issues and initiated appropriate corrective actions when adverse
prevent recurrence.  
    trends were identified. The team attended various plant meetings to observe
    management oversight and implementing functions of the corrective action process.
Additionally, the team performed control room walkdowns to assess the main control  
    These included Management Review of NCRs meetings and Unit Evaluators meetings.
room (MCR) deficiency list and to ascertain if deficiencies were entered into the CAP.
    Documents reviewed are listed in the Attachment.
Operator workarounds and operator burden screenings were reviewed, and the team  
(2) Assessment
verified compensatory measures for deficient equipment which were being implemented  
    Identification of Issues
in the field.  
    The team determined that the licensee generally had an adequate threshold for
    identifying and correcting problems as evidenced by: the relatively few deficiencies
Finally, the team reviewed site trend reports, to determine if the licensee effectively  
    identified by the NRC that had not been previously identified by the licensee during the
trended identified issues and initiated appropriate corrective actions when adverse  
    review period; the type of problems identified and corrected; the review of licensee
trends were identified. The team attended various plant meetings to observe  
                                                                                      Enclosure
management oversight and implementing functions of the corrective action process.
These included Management Review of NCRs meetings and Unit Evaluators meetings.  
Documents reviewed are listed in the Attachment.  
  (2)  
Assessment  
Identification of Issues  
The team determined that the licensee generally had an adequate threshold for  
identifying and correcting problems as evidenced by: the relatively few deficiencies  
identified by the NRC that had not been previously identified by the licensee during the  
review period; the type of problems identified and corrected; the review of licensee  


                                          7
requirements for initiating corrective action documents as described in licensee
Procedure CAP-NGGC-0200, "Corrective Action;" the management expectation that
employees were encouraged to initiate NCRs or work orders; a review of system health
Enclosure
reports; and the teams observations during plant walkdowns. However, the team
7
identified a minor violation and seven minor issues during plant walkdowns and
requirements for initiating corrective action documents as described in licensee  
document reviews where problems were not identified and entered into the CAP by the
Procedure CAP-NGGC-0200, "Corrective Action;" the management expectation that  
licensee. Trending was generally effective in monitoring and identifying plant issues;
employees were encouraged to initiate NCRs or work orders; a review of system health  
however, the team determined that not enough time had passed to assess trends or for
reports; and the teams observations during plant walkdowns. However, the team  
the licensee to develop goals and thresholds for the newly developed performance
identified a minor violation and seven minor issues during plant walkdowns and  
indicators, such as corrective maintenance backlog or preventative maintenance
document reviews where problems were not identified and entered into the CAP by the  
deferred. Site management was actively involved in the CAP and focused appropriate
licensee. Trending was generally effective in monitoring and identifying plant issues;  
attention on significant plant issues.
however, the team determined that not enough time had passed to assess trends or for  
The team identified the following minor violation:
the licensee to develop goals and thresholds for the newly developed performance  
  * 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," states, in part, that all
indicators, such as corrective maintenance backlog or preventative maintenance  
    testing required to demonstrate that structures, systems, and components will
deferred. Site management was actively involved in the CAP and focused appropriate  
    perform satisfactorily in service is identified and performed in accordance with
attention on significant plant issues.
    written test procedures. It further states that test results shall be documented and
    evaluated to assure that test requirements have been satisfied. Contrary to the
The team identified the following minor violation:  
    above, on September 30, 2009, the team identified data recorded per
   
    Procedure MST-I0412, "Waste Processing Building (WPB) Stack 5 Flow Rate
* 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," states, in part, that all  
    Monitor and Isokinetic Sampling System Calibration dated August 20, 2009," was
testing required to demonstrate that structures, systems, and components will  
    outside the allowable range and was not discovered prior to returning the WPB Vent
perform satisfactorily in service is identified and performed in accordance with  
    Stack 5 Flow Rate Monitor and the associated Wide Range Gas Monitor (WRGM) to
written test procedures. It further states that test results shall be documented and  
    service. Upon discovery, the licensee declared the WRGM inoperable and initiated
evaluated to assure that test requirements have been satisfied. Contrary to the  
    appropriate compensatory actions pending a subsequent performance of calibration
above, on September 30, 2009, the team identified data recorded per  
    Procedure MST-I0412. This failure to comply with 10 CFR Part 50, Appendix B,
Procedure MST-I0412, "Waste Processing Building (WPB) Stack 5 Flow Rate  
    Criterion XI, "Test Control," constitutes a violation of minor significance that is not
Monitor and Isokinetic Sampling System Calibration dated August 20, 2009," was  
    subject to enforcement action in accordance with the NRC's Enforcement Policy.
outside the allowable range and was not discovered prior to returning the WPB Vent  
    This issue is similar to NRCs Inspection Manual Chapter 0612, Appendix E,
Stack 5 Flow Rate Monitor and the associated Wide Range Gas Monitor (WRGM) to  
    Example 1(a), in that the data was incorrectly recorded during the procedure and
service. Upon discovery, the licensee declared the WRGM inoperable and initiated  
    there was reasonable assurance that the Flow Stack Monitor and the associated
appropriate compensatory actions pending a subsequent performance of calibration  
    WRGM remained operable as evidenced by a successful retest per licensee
Procedure MST-I0412. This failure to comply with 10 CFR Part 50, Appendix B,  
    Procedure MST-I0412. The licensee entered this issue into the CAP as
Criterion XI, "Test Control," constitutes a violation of minor significance that is not  
    NCR 358187.
subject to enforcement action in accordance with the NRC's Enforcement Policy.
The team identified the following minor issues:
This issue is similar to NRCs Inspection Manual Chapter 0612, Appendix E,  
*   The team identified a potential adverse trend in maintenance induced voiding of
Example 1(a), in that the data was incorrectly recorded during the procedure and  
    safety-related systems. Specifically, voids had been introduced during maintenance
there was reasonable assurance that the Flow Stack Monitor and the associated  
    on an emergency service water (ESW) pump, a normal service water pump, a
WRGM remained operable as evidenced by a successful retest per licensee  
    containment spray pump, and an auxiliary feedwater pump. No operability issues
Procedure MST-I0412. The licensee entered this issue into the CAP as  
    exist for these pumps. The licensee entered this issue into the CAP as NCR
NCR 358187.  
    356943.
*   Nuclear Condition Report 357122 was written to address refrigerant/oil leakage on
The team identified the following minor issues:  
    Essential Services Chiller B. Per Procedure CAP-NGGC-0200, this NCR should
                                                                                    Enclosure
*  
The team identified a potential adverse trend in maintenance induced voiding of  
safety-related systems. Specifically, voids had been introduced during maintenance  
on an emergency service water (ESW) pump, a normal service water pump, a  
containment spray pump, and an auxiliary feedwater pump. No operability issues  
exist for these pumps. The licensee entered this issue into the CAP as NCR  
356943.  
*  
Nuclear Condition Report 357122 was written to address refrigerant/oil leakage on  
Essential Services Chiller B. Per Procedure CAP-NGGC-0200, this NCR should  


                                        8
  have been routed to the MCR so the licensee could appropriately explore any impact
  upon operability. The licensee identified that the NCR had not been properly routed
  to the MCR and took corrective action. However, the licensee failed to identify that
Enclosure
  the NCR not being properly routed to the MCR was an adverse condition. Following
8
  discussions with the inspection team, the licensee concluded that not routing the
have been routed to the MCR so the licensee could appropriately explore any impact  
  NCR to the MCR was an adverse condition and entered the issue into the CAP as
upon operability. The licensee identified that the NCR had not been properly routed  
  NCR 357595.
to the MCR and took corrective action. However, the licensee failed to identify that  
* Emergency Diesel Generator A Frequency Transducer failed on
the NCR not being properly routed to the MCR was an adverse condition. Following  
  September 11, 2009; however, NCR 247241 was not written until nine days after the
discussions with the inspection team, the licensee concluded that not routing the  
  failure. Procedure CAP-NGGC-0200 requires an NCR to be written promptly. There
NCR to the MCR was an adverse condition and entered the issue into the CAP as  
  was no impact to having this NCR written late. The licensee entered this issue into
NCR 357595.  
  the CAP as NCR 358348.
* The team reviewed the MCR logs for radiation monitor failures and discovered
*  
  Channel 2 of Radiation Monitor RM-3567ASA was declared inoperable on
Emergency Diesel Generator A Frequency Transducer failed on  
  June 8, 2009. During troubleshooting efforts, the licensee discovered that the
September 11, 2009; however, NCR 247241 was not written until nine days after the  
  Channel 2 detector had failed. The team questioned the licensee and discovered an
failure. Procedure CAP-NGGC-0200 requires an NCR to be written promptly. There  
  NCR was not initiated to document this event. Not entering this issue into CAP had
was no impact to having this NCR written late. The licensee entered this issue into  
  no effect on plant equipment. The licensee entered this issue into the CAP as NCR
the CAP as NCR 358348.  
  358412.
* During a walkdown of the RHR Trains A and B with the licensee, the inspector
*  
  identified multiple deficiencies which required entry into the CAP. The licensee
The team reviewed the MCR logs for radiation monitor failures and discovered  
  initiated NCR 355964 for obsolete testing devices remaining on motor operated valve
Channel 2 of Radiation Monitor RM-3567ASA was declared inoperable on  
  actuators. The licensee initiated NCR 355989 for both RHR pump vibration
June 8, 2009. During troubleshooting efforts, the licensee discovered that the  
  monitoring cables not enclosed in flexible conduit as per design. The licensee
Channel 2 detector had failed. The team questioned the licensee and discovered an  
  entered two other conditions into the CAP via work requests (WR): WR 399084 for
NCR was not initiated to document this event. Not entering this issue into CAP had  
  boric acid staining below 1RH-30 (RHR A Heat Exchanger Discharge Valve) and WR
no effect on plant equipment. The licensee entered this issue into the CAP as NCR  
  399087 for boric acid on 1SI-359 (LHSI Supply Isolation Valve). Lastly, the licensee
358412.  
  initiated WR 399078 for a minor grease leak on 1SI-341 (RHR B Shutdown Cooling
  Isolation Valve). The team determined that none of these issues impacted
*  
  operability of the RHR system.
During a walkdown of the RHR Trains A and B with the licensee, the inspector  
* The MCR annunciator inverter power transfer setpoints were erroneously set to
identified multiple deficiencies which required entry into the CAP. The licensee  
  104 Vdc/Vac during replacement in July 2008. This value was below the plant
initiated NCR 355964 for obsolete testing devices remaining on motor operated valve  
  drawing and vendor recommended setpoint of 120 +/- 10% Vdc/Vac. The licensee
actuators. The licensee initiated NCR 355989 for both RHR pump vibration  
  entered this issue into the CAP as NCR 355911, determined there was no current
monitoring cables not enclosed in flexible conduit as per design. The licensee  
  impact, and initiated a compensatory measure to log inverter voltage once each shift
entered two other conditions into the CAP via work requests (WR): WR 399084 for  
  to assure that the setpoint deficiency had no impact on the functionality of the MCR
boric acid staining below 1RH-30 (RHR A Heat Exchanger Discharge Valve) and WR  
  annunciators.
399087 for boric acid on 1SI-359 (LHSI Supply Isolation Valve). Lastly, the licensee  
* A safety system outage on ESW Train A, which caused a quantitative yellow risk
initiated WR 399078 for a minor grease leak on 1SI-341 (RHR B Shutdown Cooling  
  condition was extended and scheduled to overlap a qualitative yellow risk condition.
Isolation Valve). The team determined that none of these issues impacted  
  After this condition was identified, the licensee delayed the qualitative yellow risk
operability of the RHR system.  
  condition to prevent overlapping yellow risk conditions. The licensees
  Procedure WCM-001, "On-Line Maintenance Risk Management," offered no
*  
                                                                                Enclosure
The MCR annunciator inverter power transfer setpoints were erroneously set to  
104 Vdc/Vac during replacement in July 2008. This value was below the plant  
drawing and vendor recommended setpoint of 120 +/- 10% Vdc/Vac. The licensee  
entered this issue into the CAP as NCR 355911, determined there was no current  
impact, and initiated a compensatory measure to log inverter voltage once each shift  
to assure that the setpoint deficiency had no impact on the functionality of the MCR  
annunciators.  
*  
A safety system outage on ESW Train A, which caused a quantitative yellow risk  
condition was extended and scheduled to overlap a qualitative yellow risk condition.
After this condition was identified, the licensee delayed the qualitative yellow risk  
condition to prevent overlapping yellow risk conditions. The licensees  
Procedure WCM-001, "On-Line Maintenance Risk Management," offered no  


                                          9
    guidance to consider the combined effect of quantitative and qualitative risk
    conditions. The licensee entered this issue into the CAP as NCR 356048.
Prioritization and Evaluation of Issues
Enclosure
Based on the review of audits conducted by the licensee and the assessment conducted
9
by the inspection team during the onsite period, the team concluded that problems were
guidance to consider the combined effect of quantitative and qualitative risk  
generally prioritized and evaluated in accordance with the licensees CAP procedures as
conditions. The licensee entered this issue into the CAP as NCR 356048.  
described in the NCR Processing Guidelines in Procedure CAP-NGGC-0200. Each
NCR written was assigned a priority level at the NCR review meetings. Management
Prioritization and Evaluation of Issues  
reviews of NCRs were thorough and adequate consideration was given to system or
component operability and associated plant risk.
Based on the review of audits conducted by the licensee and the assessment conducted  
The team determined that the station had conducted root cause and apparent cause
by the inspection team during the onsite period, the team concluded that problems were  
analyses in compliance with the licensees CAP procedures, and assigned cause
generally prioritized and evaluated in accordance with the licensees CAP procedures as  
determinations were appropriate considering the significance of the issues being
described in the NCR Processing Guidelines in Procedure CAP-NGGC-0200. Each  
evaluated. A variety of causal-analysis techniques were used depending on the type
NCR written was assigned a priority level at the NCR review meetings. Management  
and complexity of the issue consistent with licensee Procedure CAP-NGGC-0205.
reviews of NCRs were thorough and adequate consideration was given to system or  
The team determined that generally, the licensee had performed evaluations that were
component operability and associated plant risk.  
technically accurate and of sufficient depth. The team further determined that
operability, reportability, and degraded or non-conforming condition determinations had
The team determined that the station had conducted root cause and apparent cause  
been completed consistent with the guidance contained in Procedures CAP-NGGC-0200
analyses in compliance with the licensees CAP procedures, and assigned cause  
and OPS-NGGC-1305, "Operability Determinations." However, the team identified one
determinations were appropriate considering the significance of the issues being  
unresolved item (URI) which is documented in Section 4OA2.a(3)(iii) of this report, and
evaluated. A variety of causal-analysis techniques were used depending on the type  
two minor issues in this assessment area during the review of NCRs:
and complexity of the issue consistent with licensee Procedure CAP-NGGC-0205.  
*   Emergency Diesel Generator A Frequency Transducer failed on
    September 11, 2009; however, the licensee determined a reportability review was
The team determined that generally, the licensee had performed evaluations that were  
    not required for the failed component as documented in NCR 247241.
technically accurate and of sufficient depth. The team further determined that  
    Procedure CAP-NGGC-0200 requires NCRs be reviewed for reportability. The
operability, reportability, and degraded or non-conforming condition determinations had  
    licensee performed a preliminary review and determined that the frequency
been completed consistent with the guidance contained in Procedures CAP-NGGC-0200  
    transducer failed in a conservative direction. The licensee entered this issue into the
and OPS-NGGC-1305, "Operability Determinations." However, the team identified one  
    CAP as NCR 357786.
unresolved item (URI) which is documented in Section 4OA2.a(3)(iii) of this report, and  
*   Nuclear Condition Report 263267 investigated the degraded grid time delay relays
two minor issues in this assessment area during the review of NCRs:  
    for the safety-related 6.9 kilovolt (kV) Busses 1A-SA and 1B-SB that failed their
    as-found TS surveillance test during refueling outage (RFO) 14. The team
*  
    questioned the licensee on their selected cause for the relay failures and determined
Emergency Diesel Generator A Frequency Transducer failed on  
    that the defective relays were not quarantined or evaluated, following their
September 11, 2009; however, the licensee determined a reportability review was  
    replacement, in an effort to validate the selected cause. The licensee entered this
not required for the failed component as documented in NCR 247241.
    issue into the CAP as NCR 358290 to improve the quarantine process for defective
Procedure CAP-NGGC-0200 requires NCRs be reviewed for reportability. The  
    parts. The team concluded that the selected cause was adequate based on
licensee performed a preliminary review and determined that the frequency  
    available information and that corrective action to replace the failed relays with a
transducer failed in a conservative direction. The licensee entered this issue into the  
    different type of relay was adequate.
CAP as NCR 357786.  
                                                                                  Enclosure
*  
Nuclear Condition Report 263267 investigated the degraded grid time delay relays  
for the safety-related 6.9 kilovolt (kV) Busses 1A-SA and 1B-SB that failed their  
as-found TS surveillance test during refueling outage (RFO) 14. The team  
questioned the licensee on their selected cause for the relay failures and determined  
that the defective relays were not quarantined or evaluated, following their  
replacement, in an effort to validate the selected cause. The licensee entered this  
issue into the CAP as NCR 358290 to improve the quarantine process for defective  
parts. The team concluded that the selected cause was adequate based on  
available information and that corrective action to replace the failed relays with a  
different type of relay was adequate.  


                                          10
Effectiveness of Corrective Actions
Based on a review of corrective action documents, interviews with licensee staff, and
verification of completed corrective actions, the team determined that overall, corrective
Enclosure
actions were timely, commensurate with the safety significance of the issues, and
10
effective, in that conditions adverse to quality were corrected in accordance with the
Effectiveness of Corrective Actions  
licensee CAP procedures. For the significant conditions adverse to quality reviewed,
generally the corrective actions directly addressed the cause and effectively prevented
Based on a review of corrective action documents, interviews with licensee staff, and  
recurrence, as evidenced by a review of performance indicators, NCRs, and discussions
verification of completed corrective actions, the team determined that overall, corrective  
with licensee staff that demonstrated that the significant conditions adverse to quality
actions were timely, commensurate with the safety significance of the issues, and  
had not recurred. Effectiveness reviews for corrective actions to preclude recurrence
effective, in that conditions adverse to quality were corrected in accordance with the  
(CAPRs) were scheduled consistent with licensee procedures. However, during the
licensee CAP procedures. For the significant conditions adverse to quality reviewed,  
review of NCRs, the team identified two violations of NRC requirements and an
generally the corrective actions directly addressed the cause and effectively prevented  
additional minor issue regarding adequacy and timeliness of corrective actions.
recurrence, as evidenced by a review of performance indicators, NCRs, and discussions  
The team identified the following two violations:
with licensee staff that demonstrated that the significant conditions adverse to quality  
  * Between July 2009 and the present, Containment Spray Additive System Eductor A
had not recurred. Effectiveness reviews for corrective actions to preclude recurrence  
    was found three times and Eductor B was found once outside of the TS 3.6.2.2 flow
(CAPRs) were scheduled consistent with licensee procedures. However, during the  
    band. This issue was previously identified as a significant condition adverse to
review of NCRs, the team identified two violations of NRC requirements and an  
    quality in January 2008, but the corrective actions taken failed to preclude
additional minor issue regarding adequacy and timeliness of corrective actions.  
    recurrence. The team identified one finding for the failure to identify the cause and
    take CAPR of a significant condition adverse to quality for both containment spray
The team identified the following two violations:  
    additive system eductors being outside of the TS flow band as documented in
   
    Section 4OA2.a(3)(i). The licensee entered this issue into the CAP as NCR 356873.
* Between July 2009 and the present, Containment Spray Additive System Eductor A  
*   Between May 27, 1997 and September 29, 2007, Main Steam Isolation Valve MS-82
was found three times and Eductor B was found once outside of the TS 3.6.2.2 flow  
    close stroke time exhibited a degrading trend towards the TS limit without sufficient
band. This issue was previously identified as a significant condition adverse to  
    corrective actions to prevent failure. This resulted in MS-82 exceeding the five-
quality in January 2008, but the corrective actions taken failed to preclude  
    second stroke time limit required in TS 3.7.1.5. The team identified one finding for
recurrence. The team identified one finding for the failure to identify the cause and  
    failure to correct a condition adverse to quality in a timely manner as documented in
take CAPR of a significant condition adverse to quality for both containment spray  
    Section 4OA2.a(3)(ii). The licensee entered this issue into the CAP as NCR 358464.
additive system eductors being outside of the TS flow band as documented in  
The team identified the following minor issue:
Section 4OA2.a(3)(i). The licensee entered this issue into the CAP as NCR 356873.  
*   Nuclear Condition Report 290961 evaluated the failure of the main condenser
    expansion joint that caused a loss of vacuum and resulted in a manual trip of the
*  
    unit. This issue was discussed in more detail in LER 2008-002-00. The team
Between May 27, 1997 and September 29, 2007, Main Steam Isolation Valve MS-82  
    determined that while the corrective actions were generally adequate, the expansion
close stroke time exhibited a degrading trend towards the TS limit without sufficient  
    joint inspection instructions do not contain specific acceptance criteria. Specific
corrective actions to prevent failure. This resulted in MS-82 exceeding the five-
    acceptance criteria for inspecting for dry rot, cracking, splitting or other signs of
second stroke time limit required in TS 3.7.1.5. The team identified one finding for  
    degradation is necessary to ensure an objective review to determine if results are
failure to correct a condition adverse to quality in a timely manner as documented in  
    satisfactory. The team determined that the potential still exists for degradation not
Section 4OA2.a(3)(ii). The licensee entered this issue into the CAP as NCR 358464.  
    being properly identified. The licensee entered this issue into the CAP as NCR
    358345.
The team identified the following minor issue:  
                                                                                    Enclosure
*  
Nuclear Condition Report 290961 evaluated the failure of the main condenser  
expansion joint that caused a loss of vacuum and resulted in a manual trip of the  
unit. This issue was discussed in more detail in LER 2008-002-00. The team  
determined that while the corrective actions were generally adequate, the expansion  
joint inspection instructions do not contain specific acceptance criteria. Specific  
acceptance criteria for inspecting for dry rot, cracking, splitting or other signs of  
degradation is necessary to ensure an objective review to determine if results are  
satisfactory. The team determined that the potential still exists for degradation not  
being properly identified. The licensee entered this issue into the CAP as NCR  
358345.  


                                              11
(3) Findings
(i) Failure to Preclude Repetition of a Significant Condition Adverse to Quality for Both
    Containment Spray Additive System Eductors Being Outside of the Technical
Enclosure
    Specification Flow Band
11
    Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,
  (3)  
    Appendix B, Criterion XVI, "Corrective Action," for the licensees failure to identify the
Findings  
    cause and take CAPR of a significant condition adverse to quality for both containment
    spray additive system eductors being outside of the TS flow band, which resulted in
(i)  
    Eductor A found three times and Eductor B found once outside of the TS 3.6.2.2 flow
Failure to Preclude Repetition of a Significant Condition Adverse to Quality for Both  
    band between July 2009 and the present.
Containment Spray Additive System Eductors Being Outside of the Technical  
    Description. Between November 2007 and May 2008, the containment spray additive
Specification Flow Band  
    system eductors were found outside of the TS 3.6.2.2 flow band seven times. In
    January 2008, the licensee determined that this was a significant condition adverse to
Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,  
    quality and performed a root cause investigation. During the course of their
Appendix B, Criterion XVI, "Corrective Action," for the licensees failure to identify the  
    investigation, the licensee identified two root causes: entrapped air in the system and
cause and take CAPR of a significant condition adverse to quality for both containment  
    inadequate system design. As CAPRs, the licensee established a procedure to identify
spray additive system eductors being outside of the TS flow band, which resulted in  
    air voids in the system, revised the operations procedure to prevent the eductors from
Eductor A found three times and Eductor B found once outside of the TS 3.6.2.2 flow  
    being operated with the suction line isolated, and installed more stable throttle valves in
band between July 2009 and the present.  
    the suction line. The licensee reported the condition to the NRC in May 2008 as
    LER 2008-01-00. This LER was closed as a Licensee Identified Violation (LIV) in
Description. Between November 2007 and May 2008, the containment spray additive  
    Inspection Report 05000400/2008004.
system eductors were found outside of the TS 3.6.2.2 flow band seven times. In  
    The purpose of the eductor is to introduce sodium hydroxide (NaOH) into the
January 2008, the licensee determined that this was a significant condition adverse to  
    containment spray (CT) system flow during a loss of coolant accident. If there is too little
quality and performed a root cause investigation. During the course of their  
    eductor flow, not enough NaOH would be present and the iodine scrubbing capability of
investigation, the licensee identified two root causes: entrapped air in the system and  
    the CT system would be reduced. If too much NaOH is present, CT flow pH could rise
inadequate system design. As CAPRs, the licensee established a procedure to identify  
    high enough to increase degradation of aluminum in containment. This could result in
air voids in the system, revised the operations procedure to prevent the eductors from  
    increased debris accumulating on the emergency core cooling system recirculation
being operated with the suction line isolated, and installed more stable throttle valves in  
    sump screens and reducing performance of the emergency core cooling system. During
the suction line. The licensee reported the condition to the NRC in May 2008 as  
    their previous investigation, the licensee determined that they had experienced eductor
LER 2008-01-00. This LER was closed as a Licensee Identified Violation (LIV) in  
    flows both above and below the TS flow band.
Inspection Report 05000400/2008004.  
    The team reviewed the licensees implementation of the CAPRs, and determined the
    CAPRs were ineffective at precluding repetition of a significant condition adverse to
The purpose of the eductor is to introduce sodium hydroxide (NaOH) into the  
    quality since the eductor flows were discovered outside of the TS band between
containment spray (CT) system flow during a loss of coolant accident. If there is too little  
    July 2009 and the present. On three occasions flow was below the TS band, and on one
eductor flow, not enough NaOH would be present and the iodine scrubbing capability of  
    occasion flow was above the TS band. The licensee took immediate corrective actions
the CT system would be reduced. If too much NaOH is present, CT flow pH could rise  
    to adjust flow back into the TS band. Additionally, the licensee developed a
high enough to increase degradation of aluminum in containment. This could result in  
    compensatory measure to dispatch a dedicated operator to adjust flow as necessary in
increased debris accumulating on the emergency core cooling system recirculation  
    the case of CT initiation. The licensee initiated NCR 356873, reopened the root cause
sump screens and reducing performance of the emergency core cooling system. During  
    investigation, is reevaluating the cause determination that was performed in 2008, and is
their previous investigation, the licensee determined that they had experienced eductor  
    developing additional CAPRs to address the root cause.
flows both above and below the TS flow band.  
    Analysis. The performance deficiency associated with this finding involved the
    licensees failure to identify the cause and take CAPR of a significant condition adverse
The team reviewed the licensees implementation of the CAPRs, and determined the  
                                                                                      Enclosure
CAPRs were ineffective at precluding repetition of a significant condition adverse to  
quality since the eductor flows were discovered outside of the TS band between  
July 2009 and the present. On three occasions flow was below the TS band, and on one  
occasion flow was above the TS band. The licensee took immediate corrective actions  
to adjust flow back into the TS band. Additionally, the licensee developed a  
compensatory measure to dispatch a dedicated operator to adjust flow as necessary in  
the case of CT initiation. The licensee initiated NCR 356873, reopened the root cause  
investigation, is reevaluating the cause determination that was performed in 2008, and is  
developing additional CAPRs to address the root cause.  
Analysis. The performance deficiency associated with this finding involved the  
licensees failure to identify the cause and take CAPR of a significant condition adverse  


                                              12
    to quality, resulting in both containment spray additive system eductors being outside of
    the TS 3.6.2.2 flow band. The finding is more than minor because it is associated with
    the design control attribute of the Barrier Integrity Cornerstone and affects the
Enclosure
    cornerstone objective of providing reasonable assurance that physical design barriers,
12
    such as the iodine scrubbing capability of the containment spray additive system
to quality, resulting in both containment spray additive system eductors being outside of  
    eductors, will protect the public from radionuclide releases caused by accidents or
the TS 3.6.2.2 flow band. The finding is more than minor because it is associated with  
    events. Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and
the design control attribute of the Barrier Integrity Cornerstone and affects the  
    Characterization of Findings," the finding was determined to have a very low safety
cornerstone objective of providing reasonable assurance that physical design barriers,  
    significance because it did not represent a degradation of the radiological barrier
such as the iodine scrubbing capability of the containment spray additive system  
    function provided for the control room, auxiliary building, or spent fuel pool; the finding
eductors, will protect the public from radionuclide releases caused by accidents or  
    did not represent a degradation of the barrier function of the control room against smoke
events. Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and  
    or a toxic atmosphere; the finding did not represent an actual open pathway in the
Characterization of Findings," the finding was determined to have a very low safety  
    physical integrity of reactor containment; and the finding did not involve an actual
significance because it did not represent a degradation of the radiological barrier  
    reduction in function of the hydrogen igniters in the reactor containment. The finding has
function provided for the control room, auxiliary building, or spent fuel pool; the finding  
    a cross-cutting aspect in the area of problem identification and resolution associated with
did not represent a degradation of the barrier function of the control room against smoke  
    the corrective action program because the licensee did not thoroughly evaluate
or a toxic atmosphere; the finding did not represent an actual open pathway in the  
    problems such that the resolutions address causes and extent of conditions, as
physical integrity of reactor containment; and the finding did not involve an actual  
    necessary, and for significant problems, conduct effectiveness reviews of corrective
reduction in function of the hydrogen igniters in the reactor containment. The finding has  
    actions to ensure that the problems are resolved (P.1(c)).
a cross-cutting aspect in the area of problem identification and resolution associated with  
    Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,
the corrective action program because the licensee did not thoroughly evaluate  
    Criterion XVI, "Corrective Action," requires, in part, that in the case of a significant
problems such that the resolutions address causes and extent of conditions, as  
    condition adverse to quality, the measures taken shall assure that the cause of the
necessary, and for significant problems, conduct effectiveness reviews of corrective  
    condition is determined and corrective action should preclude repetition. Contrary to this
actions to ensure that the problems are resolved (P.1(c)).  
    requirement, the licensee failed to identify the cause and take CAPR of both
    containment spray additive system eductors being outside of the TS flow band.
Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,  
    Specifically, between July 2009 and the present, the violation occurred when Eductor A
Criterion XVI, "Corrective Action," requires, in part, that in the case of a significant  
    was found three times and Eductor B was found once outside of the TS 3.6.2.2 flow
condition adverse to quality, the measures taken shall assure that the cause of the  
    band.
condition is determined and corrective action should preclude repetition. Contrary to this  
    The licensee took immediate corrective action to throttle eductor flow to within the TS
requirement, the licensee failed to identify the cause and take CAPR of both  
    band, and is developing CAPRs. Because the finding is of very low safety significance
containment spray additive system eductors being outside of the TS flow band.
    and has been entered into the licensees CAP as NCR 356873, this violation is being
Specifically, between July 2009 and the present, the violation occurred when Eductor A  
    treated as an NCV consistent with Section VI.A.1 of the Enforcement Policy:
was found three times and Eductor B was found once outside of the TS 3.6.2.2 flow  
    NCV 05000400/ 2009006-01, "Failure to Preclude Repetition of a Significant Condition
band.  
    Adverse to Quality for Both Containment Spray Additive System Eductors Being Outside
    of the Technical Specification Flow Band."
The licensee took immediate corrective action to throttle eductor flow to within the TS  
(ii) Failure to Correct a Condition Adverse to Quality Involving a Main Steam Isolation Valve
band, and is developing CAPRs. Because the finding is of very low safety significance  
    Degrading Trend Before Valve Failure
and has been entered into the licensees CAP as NCR 356873, this violation is being  
    Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,
treated as an NCV consistent with Section VI.A.1 of the Enforcement Policy:
    Appendix B, Criterion XVI, "Corrective Action," for the licensees failure to correct a
NCV 05000400/ 2009006-01, "Failure to Preclude Repetition of a Significant Condition  
    condition adverse to quality in a timely manner, which resulted in MS-82 exceeding the
Adverse to Quality for Both Containment Spray Additive System Eductors Being Outside  
    TS stroke time limit.
of the Technical Specification Flow Band."  
    Description. On September 29, 2007, Valve MS-82 failed surveillance test
    Procedure OST-1046, "Main Steam Isolation Valve Operability Test Quarterly Interval
(ii)  
                                                                                          Enclosure
Failure to Correct a Condition Adverse to Quality Involving a Main Steam Isolation Valve  
Degrading Trend Before Valve Failure  
Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,  
Appendix B, Criterion XVI, "Corrective Action," for the licensees failure to correct a  
condition adverse to quality in a timely manner, which resulted in MS-82 exceeding the  
TS stroke time limit.  
Description. On September 29, 2007, Valve MS-82 failed surveillance test  
Procedure OST-1046, "Main Steam Isolation Valve Operability Test Quarterly Interval  


                                          13
Mode 3 to 5," due to exceeding the close stroke time limit of five seconds. Technical
Specification Surveillance Requirement 4.7.1.5, "Main Steam Line Isolation Valves,"
requires this valve to stroke close within five seconds. The main steam isolation valves
Enclosure
are required to close to act as a barrier to a radiological release during a steam
13
generator tube rupture or to mitigate a main steam line break. The licensee declared
Mode 3 to 5," due to exceeding the close stroke time limit of five seconds. Technical  
Valve MS-82 inoperable, wrote NCR 248429, and performed WO 1120864 to repair the
Specification Surveillance Requirement 4.7.1.5, "Main Steam Line Isolation Valves,"  
valve and decrease the stroke time.
requires this valve to stroke close within five seconds. The main steam isolation valves  
The licensee had been trending the close stroke time of Valve MS-82 since
are required to close to act as a barrier to a radiological release during a steam  
December 29, 1986. The close stroke time trend started to degrade around
generator tube rupture or to mitigate a main steam line break. The licensee declared  
May 27, 1997. In May 2004, the valve was labeled low margin due to the valve stroking
Valve MS-82 inoperable, wrote NCR 248429, and performed WO 1120864 to repair the  
close at 4.74 seconds, which was approaching the five-second limit. Between May 2004
valve and decrease the stroke time.  
and RFO 13 in April 2006, the valve stroke time continued to increase so that at the start
of RFO 13 the valve stroked close at 4.96 seconds. The licensee replaced the actuator
The licensee had been trending the close stroke time of Valve MS-82 since  
of the valve; however, the as-left valve stroke time at the end of RFO 13 was still near
December 29, 1986. The close stroke time trend started to degrade around  
the TS limit at 4.92 seconds.
May 27, 1997. In May 2004, the valve was labeled low margin due to the valve stroking  
The licensee developed contingency WO 1120864 for RFO 14, to gain stroke time
close at 4.74 seconds, which was approaching the five-second limit. Between May 2004  
margin by adjusting the air operated valve hydraulic system flow control valve. During
and RFO 13 in April 2006, the valve stroke time continued to increase so that at the start  
RFO 14, on September 29, 2007, Valve MS-82 failed the stroke time close test by
of RFO 13 the valve stroked close at 4.96 seconds. The licensee replaced the actuator  
stroking at 5.17 seconds. The licensee implemented contingency WO 1120864.
of the valve; however, the as-left valve stroke time at the end of RFO 13 was still near  
The team reviewed NCR 248429 and the close stroke time trend for Valve MS-82. The
the TS limit at 4.92 seconds.  
team questioned why the degrading trend since 1997 had not been identified, and an
NCR had not been written to correct the condition. The team determined that unlike the
The licensee developed contingency WO 1120864 for RFO 14, to gain stroke time  
other valves in the in-service testing program, no process or procedure existed to
margin by adjusting the air operated valve hydraulic system flow control valve. During  
identify a degrading trend on a main steam isolation valve, write a NCR, and correct the
RFO 14, on September 29, 2007, Valve MS-82 failed the stroke time close test by  
condition before valve failure. The team determined this issue was indicative of current
stroking at 5.17 seconds. The licensee implemented contingency WO 1120864.  
plant performance since no process or procedure currently exists.
The team questioned that with the degrading trend nearing the close stroke time limit,
The team reviewed NCR 248429 and the close stroke time trend for Valve MS-82. The  
why effective maintenance was not performed in RFO 13 to ensure the valve would not
team questioned why the degrading trend since 1997 had not been identified, and an  
exceed the TS close stroke time before RFO 14. The team reviewed the surveillance
NCR had not been written to correct the condition. The team determined that unlike the  
test performed on April 8, 2006, and noted that the licensee was still in Mode 5 where
other valves in the in-service testing program, no process or procedure existed to  
maintenance could have been performed on the valve. However, the team noted that
identify a degrading trend on a main steam isolation valve, write a NCR, and correct the  
the surveillance test results were not reviewed until April 11, 2006, when the plant was in
condition before valve failure. The team determined this issue was indicative of current  
Mode 3, when maintenance could not be performed on the valve. The team also
plant performance since no process or procedure currently exists.
reviewed NCR 248429 that stated "It consistently has been a conscious decision not to
adjust these valves to gain stroke time margin because of the ensuing post maintenance
The team questioned that with the degrading trend nearing the close stroke time limit,  
test required." This NCR also stated that the decision not to perform maintenance was
why effective maintenance was not performed in RFO 13 to ensure the valve would not  
deemed to be an acceptable risk. Not performing effective maintenance on the
exceed the TS close stroke time before RFO 14. The team reviewed the surveillance  
degrading stroke time close trend for Valve MS-82 led to the failure of this valve in
test performed on April 8, 2006, and noted that the licensee was still in Mode 5 where  
RFO 14. The licensee wrote NCR 358464 to address why corrective actions were not
maintenance could have been performed on the valve. However, the team noted that  
taken before Valve MS-82 failed.
the surveillance test results were not reviewed until April 11, 2006, when the plant was in  
  Analysis. The performance deficiency associated with this finding involved the
Mode 3, when maintenance could not be performed on the valve. The team also  
licensees failure to correct a condition adverse to quality in a timely manner, which
reviewed NCR 248429 that stated "It consistently has been a conscious decision not to  
resulted in Valve MS-82 exceeding the TS stroke time limit. This finding is more than
adjust these valves to gain stroke time margin because of the ensuing post maintenance  
                                                                                  Enclosure
test required." This NCR also stated that the decision not to perform maintenance was  
deemed to be an acceptable risk. Not performing effective maintenance on the  
degrading stroke time close trend for Valve MS-82 led to the failure of this valve in  
RFO 14. The licensee wrote NCR 358464 to address why corrective actions were not  
taken before Valve MS-82 failed.  
   
Analysis. The performance deficiency associated with this finding involved the  
licensees failure to correct a condition adverse to quality in a timely manner, which  
resulted in Valve MS-82 exceeding the TS stroke time limit. This finding is more than  


                                                14
      minor because it is associated with the containment barrier performance attribute of the
      Barrier Integrity Cornerstone and affects the cornerstone objective of providing
      reasonable assurance that physical design barriers, such as the main steam isolation
Enclosure
      valve radiological release barrier required for a steam generator tube rupture, protect
14
      the public from radionuclide releases caused by accidents or events. Using Manual
minor because it is associated with the containment barrier performance attribute of the  
      Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the
Barrier Integrity Cornerstone and affects the cornerstone objective of providing  
      finding was determined to have a very low safety significance because it did not
reasonable assurance that physical design barriers, such as the main steam isolation  
      represent a degradation of the radiological barrier function provided for the control room,
valve radiological release barrier required for a steam generator tube rupture, protect  
      auxiliary building, or spent fuel pool; the finding did not represent a degradation of the
the public from radionuclide releases caused by accidents or events. Using Manual  
      barrier function of the control room against smoke or a toxic atmosphere; the finding did
Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the  
      not represent an actual open pathway in the physical integrity of reactor containment;
finding was determined to have a very low safety significance because it did not  
      and the finding did not involve an actual reduction in function of the hydrogen igniters in
represent a degradation of the radiological barrier function provided for the control room,  
      the reactor containment. This finding has a cross-cutting aspect in the area of human
auxiliary building, or spent fuel pool; the finding did not represent a degradation of the  
      performance associated with decision-making because the licensee did not use
barrier function of the control room against smoke or a toxic atmosphere; the finding did  
      conservative assumptions so that safety-significant decisions were verified to validate
not represent an actual open pathway in the physical integrity of reactor containment;  
      underlying assumptions and identify unintended consequences (H.1.(b)).
and the finding did not involve an actual reduction in function of the hydrogen igniters in  
      Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,
the reactor containment. This finding has a cross-cutting aspect in the area of human  
      Criterion XVI, "Corrective Action," requires, in part, that measures shall be established
performance associated with decision-making because the licensee did not use  
      to assure that conditions adverse to quality are promptly identified and corrected.
conservative assumptions so that safety-significant decisions were verified to validate  
      Contrary to this requirement, between May 27, 1997 and September 29, 2007, the
underlying assumptions and identify unintended consequences (H.1.(b)).  
      licensee failed to identify and correct a condition adverse to quality for a trend degrading
      towards the technical specification limit, without sufficient corrective actions to prevent
Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,  
      failure. This resulted in Main Steam Isolation Valve 82 exceeding the five-second stroke
Criterion XVI, "Corrective Action," requires, in part, that measures shall be established  
      time limit required in Technical Specification 3.7.1.5. Because the finding is of very low
to assure that conditions adverse to quality are promptly identified and corrected.
      safety significance and has been entered into the licensees CAP as NCR 358464, this
Contrary to this requirement, between May 27, 1997 and September 29, 2007, the  
      violation is being treated as an NCV consistent with Section VI.A.1 of the Enforcement
licensee failed to identify and correct a condition adverse to quality for a trend degrading  
      Policy: NCV 05000400/2009006-02, "Failure to Correct a Condition Adverse to Quality
towards the technical specification limit, without sufficient corrective actions to prevent  
      Involving a Main Steam Isolation Valve Degrading Trend Before Valve Failure."
failure. This resulted in Main Steam Isolation Valve 82 exceeding the five-second stroke  
(iii) Unresolved Item Associated With the Evaluation of the Failure of Emergency Service
time limit required in Technical Specification 3.7.1.5. Because the finding is of very low  
      Water Valve 271
safety significance and has been entered into the licensees CAP as NCR 358464, this  
      Introduction. The inspectors identified a URI associated with the evaluation of the failure
violation is being treated as an NCV consistent with Section VI.A.1 of the Enforcement  
      of ESW Auxiliary Reservoir Discharge Valve 271 to open on the start of ESW Pump B.
Policy: NCV 05000400/2009006-02, "Failure to Correct a Condition Adverse to Quality  
      Description. On October 19, 2007, while in Mode 5, ESW Auxiliary Reservoir Discharge
Involving a Main Steam Isolation Valve Degrading Trend Before Valve Failure."  
      Valve 271 failed to open on the start of ESW Pump B. This valve is required to open on
      the start of an ESW pump to provide a discharge path for the cooling water. Operators
(iii)  
      immediately stopped ESW Pump B and aligned normal service water to the safety
Unresolved Item Associated With the Evaluation of the Failure of Emergency Service  
      related components in Train B. The licensee determined that the auto open controls for
Water Valve 271  
      Valve SW-271 had been disabled by a clearance order for unrelated work. Although
      ESW Train B is not required to be operational in Mode 5, the components cooled by
Introduction. The inspectors identified a URI associated with the evaluation of the failure  
      ESW Train B, such as EDG B and RHR Train B, were being relied upon as protected
of ESW Auxiliary Reservoir Discharge Valve 271 to open on the start of ESW Pump B.  
      train equipment. Therefore, ESW Train B was necessary to ensure core decay heat
      removal in the event that off-site power was not available. NRC inspectors wrote a
Description. On October 19, 2007, while in Mode 5, ESW Auxiliary Reservoir Discharge  
      self-revealing NCV of TS 6.8.1, "Programs and Procedures," for an inadequate
Valve 271 failed to open on the start of ESW Pump B. This valve is required to open on  
      clearance order as documented in NRC Integrated Inspection Report
the start of an ESW pump to provide a discharge path for the cooling water. Operators  
                                                                                          Enclosure
immediately stopped ESW Pump B and aligned normal service water to the safety  
related components in Train B. The licensee determined that the auto open controls for  
Valve SW-271 had been disabled by a clearance order for unrelated work. Although  
ESW Train B is not required to be operational in Mode 5, the components cooled by  
ESW Train B, such as EDG B and RHR Train B, were being relied upon as protected  
train equipment. Therefore, ESW Train B was necessary to ensure core decay heat  
removal in the event that off-site power was not available. NRC inspectors wrote a  
self-revealing NCV of TS 6.8.1, "Programs and Procedures," for an inadequate  
clearance order as documented in NRC Integrated Inspection Report  


                                              15
    05000400/2007005. The team reviewed the evaluation performed for this NCV including
    the reportability review. The reportability review stated this condition was not reportable
    since operators were able to open this valve manually from the control room. The team
Enclosure
    questioned whether the operators would be able to open the valve within one minute,
15
    which is required to ensure cooling to the EDGs during an accident. The team also
05000400/2007005. The team reviewed the evaluation performed for this NCV including  
    determined that when the valve is manually opened by the reactor operators from the
the reportability review. The reportability review stated this condition was not reportable  
    control room, that the valve would automatically go closed due to the inadequate
since operators were able to open this valve manually from the control room. The team  
    clearance. As a result of the teams questions, the licensee wrote NCR 358062 and
questioned whether the operators would be able to open the valve within one minute,  
    determined that the failure of SW-271 to open was a MRFF. This failure did not exceed
which is required to ensure cooling to the EDGs during an accident. The team also  
    the ESW Train B maintenance rule performance criteria. The licensee determined that
determined that when the valve is manually opened by the reactor operators from the  
    this failure affected the MSPI. This condition could prevent the fulfillment of the safety
control room, that the valve would automatically go closed due to the inadequate  
    function of EDG B and RHR B that are needed to maintain the reactor in a safe
clearance. As a result of the teams questions, the licensee wrote NCR 358062 and  
    shutdown condition or to remove residual heat. The licensee wrote NCR 361821 to
determined that the failure of SW-271 to open was a MRFF. This failure did not exceed  
    address this issue. This issue is considered unresolved pending additional NRC review
the ESW Train B maintenance rule performance criteria. The licensee determined that  
    of the evaluation of the failure including the reportability review, the risk assessment, and
this failure affected the MSPI. This condition could prevent the fulfillment of the safety  
    the corrective actions: URI 05000400/2009006-03, "Unresolved Item Associated with
function of EDG B and RHR B that are needed to maintain the reactor in a safe  
    the Evaluation of the Failure of Emergency Service Water Valve 271."
shutdown condition or to remove residual heat. The licensee wrote NCR 361821 to  
b. Assessment of the Use of Operating Experience
address this issue. This issue is considered unresolved pending additional NRC review  
(1) Inspection Scope
of the evaluation of the failure including the reportability review, the risk assessment, and  
    The team examined licensee programs for reviewing industry operating experience
the corrective actions: URI 05000400/2009006-03, "Unresolved Item Associated with  
    (OE), reviewed licensees Procedure CAP-NGGC-0202, "Operating Experience
the Evaluation of the Failure of Emergency Service Water Valve 271."  
    Program," and reviewed the licensees OE database, to assess the effectiveness of how
    external and internal OE data was handled at the plant. In addition, the team selected
  b.  
    OE documents (e.g., NRC generic communications, 10 CFR Part 21 reports, LERs,
Assessment of the Use of Operating Experience  
    vendor notifications, etc.), which had been issued since August 2007, to verify whether
    the licensee had appropriately evaluated each notification for applicability to the Shearon
  (1)  
    Harris Nuclear Power Plant, and whether issues identified through these reviews were
Inspection Scope  
    entered into the CAP.
    Documents reviewed are listed in the Attachment.
The team examined licensee programs for reviewing industry operating experience  
(2) Assessment
(OE), reviewed licensees Procedure CAP-NGGC-0202, "Operating Experience  
    Based on interviews and a review of documentation related to the review of OE issues,
Program," and reviewed the licensees OE database, to assess the effectiveness of how  
    the team determined that the licensee was generally effective in screening OE for
external and internal OE data was handled at the plant. In addition, the team selected  
    applicability to the plant. Industry OE was evaluated at either the corporate or plant level
OE documents (e.g., NRC generic communications, 10 CFR Part 21 reports, LERs,  
    depending on the source and type of document. Relevant information was then
vendor notifications, etc.), which had been issued since August 2007, to verify whether  
    forwarded to the applicable department for further action or informational purposes.
the licensee had appropriately evaluated each notification for applicability to the Shearon  
    Operating experience issues requiring action were entered into the CAP for tracking and
Harris Nuclear Power Plant, and whether issues identified through these reviews were  
    closure. In addition, OE was included in apparent cause and root cause evaluations in
entered into the CAP.  
    accordance with licensee Procedure CAP-NGGC-0205.
(3) Findings
Documents reviewed are listed in the Attachment.
    No findings of significance were identified.
                                                                                        Enclosure
  (2)  
Assessment  
Based on interviews and a review of documentation related to the review of OE issues,  
the team determined that the licensee was generally effective in screening OE for  
applicability to the plant. Industry OE was evaluated at either the corporate or plant level  
depending on the source and type of document. Relevant information was then  
forwarded to the applicable department for further action or informational purposes.
Operating experience issues requiring action were entered into the CAP for tracking and  
closure. In addition, OE was included in apparent cause and root cause evaluations in  
accordance with licensee Procedure CAP-NGGC-0205.  
  (3)  
Findings  
No findings of significance were identified.  


                                              16
c. Assessment of Self-Assessments and Audits
(1) Inspection Scope
    The team reviewed audit reports and self-assessment reports, including those which
Enclosure
    focused on problem identification and resolution, to assess the thoroughness and
16
    self-criticism of the licensee's audits and self-assessments, and to verify that problems
  c.  
    identified through those activities were appropriately prioritized and entered into the CAP
Assessment of Self-Assessments and Audits  
    for resolution in accordance with licensee Procedure CAP-NGGC-0201,
    "Self-Assessment and Benchmark Programs."
  (1)  
(2) Assessment
Inspection Scope  
    The team determined that the scopes of assessments and audits were adequate.
    Self-assessments were generally detailed and critical, as evidenced by findings
The team reviewed audit reports and self-assessment reports, including those which  
    consistent with the teams independent review. Self-assessment findings related to
focused on problem identification and resolution, to assess the thoroughness and  
    issues or weaknesses were entered into the CAP and tracked to completion based on
self-criticism of the licensee's audits and self-assessments, and to verify that problems  
    the NCR priority level. Corrective actions for self-assessment findings were adequate to
identified through those activities were appropriately prioritized and entered into the CAP  
    address the issues. Generally, the licensee performed evaluations that were technically
for resolution in accordance with licensee Procedure CAP-NGGC-0201,  
    accurate. Site trend reports were thorough and a low threshold was established for
"Self-Assessment and Benchmark Programs."  
    evaluation of potential trends; however, the team determined that not enough time had
    passed to assess trends or for the licensee to develop goals and thresholds for the
  (2)  
    newly developed performance indicators, such as corrective maintenance backlog or
Assessment  
    preventative maintenance deferred. The team concluded that the self-assessments and
    audits were an effective tool to identify adverse trends.
The team determined that the scopes of assessments and audits were adequate.  
(3)  Findings
Self-assessments were generally detailed and critical, as evidenced by findings  
    No findings of significance were identified.
consistent with the teams independent review. Self-assessment findings related to  
d. Assessment of Safety-Conscious Work Environment
issues or weaknesses were entered into the CAP and tracked to completion based on  
(1) Inspection Scope
the NCR priority level. Corrective actions for self-assessment findings were adequate to  
    The team randomly interviewed 29 on-site workers from maintenance, security,
address the issues. Generally, the licensee performed evaluations that were technically  
    operations, chemistry, and engineering organizations regarding their knowledge of the
accurate. Site trend reports were thorough and a low threshold was established for  
    corrective action program at Shearon Harris and their willingness to write NCRs or raise
evaluation of potential trends; however, the team determined that not enough time had  
    safety concerns. During technical discussions with members of the plant staff, the team
passed to assess trends or for the licensee to develop goals and thresholds for the  
    conducted interviews to develop a general perspective of the safety-conscious work
newly developed performance indicators, such as corrective maintenance backlog or  
    environment at the site. The interviews were also conducted to determine if any
preventative maintenance deferred. The team concluded that the self-assessments and  
    conditions existed that would cause employees to be reluctant to raise safety concerns.
audits were an effective tool to identify adverse trends.  
    The team reviewed the licensees employee concerns program (ECP) and interviewed
    the ECP coordinator. Additionally, the team reviewed the latest Safety Culture
  (3)  
    Assessment to evaluate the thoroughness and self-criticism of the licensee's
Findings
    assessment, and to verify that problems identified were appropriately prioritized and
    entered into the CAP for resolution. Finally, the team reviewed a sample of completed
   
    ECP reports to verify that concerns were being properly reviewed and identified
No findings of significance were identified.  
    deficiencies were being resolved and entered into the CAP when appropriate.
                                                                                      Enclosure
  d.  
Assessment of Safety-Conscious Work Environment  
  (1)  
Inspection Scope  
The team randomly interviewed 29 on-site workers from maintenance, security,  
operations, chemistry, and engineering organizations regarding their knowledge of the  
corrective action program at Shearon Harris and their willingness to write NCRs or raise  
safety concerns. During technical discussions with members of the plant staff, the team  
conducted interviews to develop a general perspective of the safety-conscious work  
environment at the site. The interviews were also conducted to determine if any  
conditions existed that would cause employees to be reluctant to raise safety concerns.
The team reviewed the licensees employee concerns program (ECP) and interviewed  
the ECP coordinator. Additionally, the team reviewed the latest Safety Culture  
Assessment to evaluate the thoroughness and self-criticism of the licensee's  
assessment, and to verify that problems identified were appropriately prioritized and  
entered into the CAP for resolution. Finally, the team reviewed a sample of completed  
ECP reports to verify that concerns were being properly reviewed and identified  
deficiencies were being resolved and entered into the CAP when appropriate.  


                                              17
(2) Assessment
    Based on the interviews conducted and the NCRs reviewed, the team determined that
    licensee management emphasized the need for all employees to identify and report
Enclosure
    problems using the appropriate methods established within the administrative programs,
17
    including the CAP and ECP. These methods were readily accessible to all employees.
  (2)  
    Based on discussions conducted with a sample of plant employees from various
Assessment  
    departments, the team determined that employees felt free to raise issues, and that
    management encouraged employees to place issues into the CAP for resolution. The
Based on the interviews conducted and the NCRs reviewed, the team determined that  
    team did not identify any reluctance on the part of the licensee staff to report safety
licensee management emphasized the need for all employees to identify and report  
    concerns.
problems using the appropriate methods established within the administrative programs,  
  (3) Findings
including the CAP and ECP. These methods were readily accessible to all employees.
    No findings of significance were identified.
Based on discussions conducted with a sample of plant employees from various  
4OA6 Meetings, Including Exit
departments, the team determined that employees felt free to raise issues, and that  
    On October 2, 2009, the team presented the inspection results to Mr. Christopher Burton
management encouraged employees to place issues into the CAP for resolution. The  
    and other members of the site staff. On October 26, 2009, the team lead re-exited the
team did not identify any reluctance on the part of the licensee staff to report safety  
    inspection results concerning the unresolved item to Mr. Dave Corlett.
concerns.  
    The team confirmed that all proprietary information reviewed was returned to the
   
    licensee during the inspection.
  (3)  
ATTACHMENT: SUPPPLEMENTAL INFORMATION
Findings  
                                                                                        Enclosure
No findings of significance were identified.  
4OA6 Meetings, Including Exit  
On October 2, 2009, the team presented the inspection results to Mr. Christopher Burton  
and other members of the site staff. On October 26, 2009, the team lead re-exited the  
inspection results concerning the unresolved item to Mr. Dave Corlett.  
The team confirmed that all proprietary information reviewed was returned to the  
licensee during the inspection.  
ATTACHMENT: SUPPPLEMENTAL INFORMATION  


                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Attachment
Licensee personnel
SUPPLEMENTAL INFORMATION  
B. Bernard, Superintendent, Security
C. Burton, Vice President Harris Plant
KEY POINTS OF CONTACT  
D. Corlett, Supervisor, Licensing/Regulatory Programs
J. Dills, Manager, Operations
Licensee personnel  
J. Doorhy, Licensing
B. Bernard, Superintendent, Security  
K. Harshaw, Manager, Outage and Scheduling
C. Burton, Vice President Harris Plant  
K. Henderson, Plant General Manager
D. Corlett, Supervisor, Licensing/Regulatory Programs  
J. Jankens, Supervisor, Radiation Control
J.   Dills, Manager, Operations  
G. Kilpatrick, Training Manager
J.   Doorhy, Licensing  
P. Morales, Employee Concerns Program
K. Harshaw, Manager, Outage and Scheduling  
L. Morgan, Supervisor, Self Evaluation Unit
K. Henderson, Plant General Manager  
S. OConnor, Manager, Engineering
J. Jankens, Supervisor, Radiation Control  
M. Parker, Superintendent, Radiation Protection
G. Kilpatrick, Training Manager  
B. Parks, Manager, Nuclear Oversight Section
P. Morales, Employee Concerns Program  
J. Robinson, Superintendent, Environmental and Chemistry
L. Morgan, Supervisor, Self Evaluation Unit  
H. Szews, CAP Coordinator
S. OConnor, Manager, Engineering  
J. Warner, Manager, Support Services
M. Parker, Superintendent, Radiation Protection  
NRC
B. Parks, Manager, Nuclear Oversight Section  
J. Austin, Senior Resident Inspector
J. Robinson, Superintendent, Environmental and Chemistry  
R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects, Region II
H. Szews, CAP Coordinator  
                      LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
J. Warner, Manager, Support Services  
Opened and Closed
05000400/2009006-01             NCV   Failure to Preclude Repetition of a Significant
NRC  
                                      Condition Adverse to Quality for Both Containment
J. Austin, Senior Resident Inspector  
                                      Spray Additive System Eductors Being Outside of the
R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects, Region II  
                                      Technical Specification Flow Band (Section
                                      4OA2.a(3)(i))
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
05000400/2009006-02             NCV   Failure to Correct a Condition Adverse to Quality
                                      Involving a Main Steam Isolation Valve Degrading
Opened and Closed  
                                      Trend Before Valve Failure (Section 4OA2.a(3)(ii))
Opened
05000400/2009006-01  
05000400/2009006-03             URI   Unresolved Item Associated with the Evaluation of the
NCV  
                                      Failure of Emergency Service Water Valve 271
Failure to Preclude Repetition of a Significant  
                                      (Section 4OA2.a(3)(iii))
Condition Adverse to Quality for Both Containment  
Closed
Spray Additive System Eductors Being Outside of the  
None
Technical Specification Flow Band (Section  
Discussed
4OA2.a(3)(i))  
None
                                                                                      Attachment
05000400/2009006-02  
NCV  
Failure to Correct a Condition Adverse to Quality  
Involving a Main Steam Isolation Valve Degrading  
Trend Before Valve Failure (Section 4OA2.a(3)(ii))  
Opened  
05000400/2009006-03  
URI  
Unresolved Item Associated with the Evaluation of the  
Failure of Emergency Service Water Valve 271  
(Section 4OA2.a(3)(iii))  
Closed  
None  
Discussed  
None  


                              LIST OF DOCUMENTS REVIEWED
Procedures
Attachment
ADM-NGGC-0113, Performance Planning and Monitoring, Revision 0
LIST OF DOCUMENTS REVIEWED  
ADM-NGGC-0101, Maintenance Rule Program, Revision 20
ADM-NGGC-0104, Work Management Process, Revision 33
Procedures  
AP-013, Plant Nuclear Safety Committee, Revision 34
ADM-NGGC-0113, Performance Planning and Monitoring, Revision 0  
AP-930, Plant Observation Program, Revision 10
ADM-NGGC-0101, Maintenance Rule Program, Revision 20  
AOP-022, Loss of Service Water, Revision 29
ADM-NGGC-0104, Work Management Process, Revision 33  
OPS-NGGC-1305 Operability Determinations, Revision 1
AP-013, Plant Nuclear Safety Committee, Revision 34  
CAP-NGGC-0200, Corrective Action Program, Revision 27
AP-930, Plant Observation Program, Revision 10  
CAP-NGGC-0201, Self Assessment and Benchmark Programs, Revision 12
AOP-022, Loss of Service Water, Revision 29  
CAP-NGGC-0202, Operating Experience Program, Revision 15
OPS-NGGC-1305 Operability Determinations, Revision 1  
CAP-NGGC-0205, Significant Adverse Condition Investigations and Adverse Condition
CAP-NGGC-0200, Corrective Action Program, Revision 27  
        Investigations - Increased Rigor, Revision 9
CAP-NGGC-0201, Self Assessment and Benchmark Programs, Revision 12  
CAP-NGGC-0206, Corrective Action Program Trending and Analysis, Revision 3
CAP-NGGC-0202, Operating Experience Program, Revision 15  
NOS-NGGC-0400, Employee Concerns Program, Revision 0
CAP-NGGC-0205, Significant Adverse Condition Investigations and Adverse Condition  
EGR-NGGC-0010, System & Component Trending Program and System Notebooks,
Investigations - Increased Rigor, Revision 9  
        Revision 13
CAP-NGGC-0206, Corrective Action Program Trending and Analysis, Revision 3  
ISI-801, Inservice Testing of Valves, Revision 47
NOS-NGGC-0400, Employee Concerns Program, Revision 0  
HESS Standards, Revision 5
EGR-NGGC-0010, System & Component Trending Program and System Notebooks,  
OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,
Revision 13  
        Revision 12
ISI-801, Inservice Testing of Valves, Revision 47  
PLP-624, Mechanical Equipment Qualification Program, Revision 18
HESS Standards, Revision 5  
OP-148, Essential Services Chilled Water System, Revisions 37 and 49
OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,  
HPS-NGGC-0003, Radiological Posting, Labeling and Surveys, Revision 14
Revision 12  
MST-E0045, 6.9 KV Emergency Bus 1A-SA and 1B-SB Under Voltage Relay Channel
PLP-624, Mechanical Equipment Qualification Program, Revision 18  
        Calibration, Revision 23
OP-148, Essential Services Chilled Water System, Revisions 37 and 49  
ADM-NGCC-0203, Preventative Maintenance and Surveillance Testing Administration,
HPS-NGGC-0003, Radiological Posting, Labeling and Surveys, Revision 14  
        Revision 13
MST-E0045, 6.9 KV Emergency Bus 1A-SA and 1B-SB Under Voltage Relay Channel  
OST-1124, Train B 6.9 KV Emergency Bus Undervoltage Trip Actuating Device Operational
Calibration, Revision 23  
        Test and Contact Check Modes 1-6, Revision 25
ADM-NGCC-0203, Preventative Maintenance and Surveillance Testing Administration,  
HPS-NGGC-1000, Radiation Protection and Conduct of Operations, Revision 0
Revision 13  
SP-013 Administrative/Support Key and Lock Control, Revision 12
OST-1124, Train B 6.9 KV Emergency Bus Undervoltage Trip Actuating Device Operational  
AP-504 Administrative Controls for Locked and Very High Radiation Areas, Revision 29
Test and Contact Check Modes 1-6, Revision 25  
PLP-511 Radiation Control and Protection Program, Revision 20
HPS-NGGC-1000, Radiation Protection and Conduct of Operations, Revision 0  
CRC-240 Plant Vent Stack 1 Effluent Sampling, Revision 11
SP-013 Administrative/Support Key and Lock Control, Revision 12  
HNPS-NGGC-0003, Radiological Posting, Labeling and Surveys, Revision 14
AP-504 Administrative Controls for Locked and Very High Radiation Areas, Revision 29  
MST-E0075, 6.9 KV Emergency Buses, 1A-SA and 1B-SB Undervoltage (Loss of Voltage)
PLP-511 Radiation Control and Protection Program, Revision 20  
        Channel Calibration, Revision 6
CRC-240 Plant Vent Stack 1 Effluent Sampling, Revision 11  
NGGM-IA-0038, Carolinas - Nuclear Generation Group Siren Maintenance, Revision 1
HNPS-NGGC-0003, Radiological Posting, Labeling and Surveys, Revision 14  
ERC-004, Environmental and Chemistry Administrative Guidelines, Revision 25
MST-E0075, 6.9 KV Emergency Buses, 1A-SA and 1B-SB Undervoltage (Loss of Voltage)  
SEC-NGGC-2120, Protection of Safeguards Information, Revision 22
Channel Calibration, Revision 6  
WCM-001, On-Line Maintenance Risk Management, Revision 20
NGGM-IA-0038, Carolinas - Nuclear Generation Group Siren Maintenance, Revision 1  
OST-1118, Containment Spray Operability Train A Quarterly Interval Modes 1-4, Revision 33
ERC-004, Environmental and Chemistry Administrative Guidelines, Revision 25  
OST-1119, Containment Spray Operability Train B Quarterly Interval Modes 1-4, Revision 35
SEC-NGGC-2120, Protection of Safeguards Information, Revision 22  
MST-I0019, Main Steam/Feedwater Flow Loop 2 Channel Calibration, Revision 16
WCM-001, On-Line Maintenance Risk Management, Revision 20  
ADM-NGGC-0104, Work Management Process, Revision 33
OST-1118, Containment Spray Operability Train A Quarterly Interval Modes 1-4, Revision 33  
OST-1119, Containment Spray Operability Train B Quarterly Interval Modes 1-4, Revision 35  
MST-I0019, Main Steam/Feedwater Flow Loop 2 Channel Calibration, Revision 16  
ADM-NGGC-0104, Work Management Process, Revision 33  
MMM-002, Corrective Maintenance, Revision 17
MMM-002, Corrective Maintenance, Revision 17
                                                                                  Attachment


                                          3
MNT-NGGC-1000, Fleet Conduct of Maintenance, Revision 0
3  
WCM-005, Work Order Prioritization Process, Revision 8
Completed Surveillance Tests
Attachment
OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,
MNT-NGGC-1000, Fleet Conduct of Maintenance, Revision 0  
        Revision 12, September 29, 2007
WCM-005, Work Order Prioritization Process, Revision 8  
OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,
        Revision 12, May 11, 2006
Completed Surveillance Tests  
MST-I0412, Waste Processing Building (WPB) Stack 5 Flow Rate Monitor and Isokinetic
OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,  
        Sampling System Calibration, August 20, 2009
Revision 12, September 29, 2007  
Action Requests/Nuclear Condition Reports
OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,  
223911         244705       245320       245633       246582           247241
Revision 12, May 11, 2006  
248429         250575       250810       262037       263421           266234
MST-I0412, Waste Processing Building (WPB) Stack 5 Flow Rate Monitor and Isokinetic  
269409         279287       279715       281217       286843           297210
Sampling System Calibration, August 20, 2009  
300052         300163       301267       315670       318483           320236
320444         323631       329044       330455       337027           338184
Action Requests/Nuclear Condition Reports  
340240         340325       230031       238372       238374           263439
223911  
263441         270215       282037       287726       249284           330423
244705  
301267         329438       331701       346484       282037           279704
245320  
358062         350078       251296       249347       357786           250810
245633  
279715         244705       249347       344729       266234           248429
246582  
249992         253347       257853       262001       262192           263486
247241  
265063         267065       267066       267080       267244           268566
248429  
269406         271452       275878       278486       280015           281538
250575  
285149         285222       290761       299832       306876           316594
250810  
319422         333716       196258       221803       222730           224208
262037  
228947         253347       314660       301267       300163           286843
263421  
280649         279988       277165       269409       251296           249347
266234  
266234         263921       250810       248429       247241           244705
269409  
246582         262037       245320       245633       281217           330455
279287  
279715         231046       303142       211360       246397           292892
279715  
332141         334996       246397       292892       334934           334167
281217  
334937         263267       334936       249331       316381           253376
286843  
245663         286104       288188       326920       310739           226843
297210  
267946         307600       340516       329378       352310           283579
300052  
274978         255529       330676       241895       261182           231941
300163  
328537         201481       229805       248378       226843           327372
301267  
301730         315269       171602       188528       191359           197522
315670  
207516         223563       225187       236248       243993           246188
318483  
247129         251191       252290       254402       258053           258053
320236  
261182         263759       270318       274708       279681           281080
320444  
291651         292337       305661       313305       323057           331371
323631  
349905         350640       351437       351623       351623           355964
329044  
355989         244576       248430       252234       252471           264812
330455  
302079         317205       317280       329488       329489           331169
337027  
333828         333830       336394       340319       310373           336342
338184  
336569         247193       251437       266063       278730           279326
340240  
                                                                                  Attachment
340325  
230031  
238372  
238374  
263439  
263441  
270215  
282037  
287726  
249284  
330423  
301267  
329438  
331701  
346484  
282037  
279704  
358062  
350078  
251296  
249347  
357786  
250810  
279715  
244705  
249347  
344729  
266234  
248429  
249992  
253347  
257853  
262001  
262192  
263486  
265063  
267065  
267066  
267080  
267244  
268566  
269406  
271452  
275878  
278486  
280015  
281538  
285149  
285222  
290761  
299832  
306876  
316594  
319422  
333716  
196258  
221803  
222730  
224208  
228947  
253347  
314660  
301267  
300163  
286843  
280649  
279988  
277165  
269409  
251296  
249347  
266234  
263921  
250810  
248429  
247241  
244705  
246582  
262037  
245320  
245633  
281217  
330455  
279715  
231046  
303142  
211360  
246397  
292892  
332141  
334996  
246397  
292892  
334934  
334167  
334937  
263267  
334936  
249331  
316381  
253376  
245663  
286104  
288188  
326920  
310739  
226843  
267946  
307600  
340516  
329378  
352310  
283579  
274978  
255529  
330676  
241895  
261182  
231941  
328537  
201481  
229805  
248378  
226843  
327372  
301730  
315269  
171602  
188528  
191359  
197522  
207516  
223563  
225187  
236248  
243993  
246188  
247129  
251191  
252290  
254402  
258053  
258053  
261182  
263759  
270318  
274708  
279681  
281080  
291651  
292337  
305661  
313305  
323057  
331371  
349905  
350640  
351437  
351623  
351623  
355964  
355989  
244576  
248430  
252234  
252471  
264812  
302079  
317205  
317280  
329488  
329489  
331169  
333828  
333830  
336394  
340319  
310373  
336342  
336569  
247193  
251437  
266063  
278730  
279326


                                          4
297789
4  
Operating Experience Action Requests
306876       317361       327306         297210         329044       337027
234055       270275       291396         291403         302656       306234
Attachment
Audits and Self-Assessment Items
297789  
07-16-SP-H, HNP Nuclear Safety Culture Assessment, June 6, 2007
H-SE-06-01, Harris Site Wide Self Evaluation, June 20, 2006
Operating Experience Action Requests
H-SE-08-01, Harris Nuclear Plant Self Evaluation and Human Performance Assessment,
306876  
        June 16, 2008
317361  
H-OP-09-01, Assessment of Harris Operations Program, September 14, 2009
327306  
H-OM-FR-09-03, Focused Review of Return to Service Plans, January 19-23, 2009
297210  
H-MC-08-01, Harris Nuclear Material and Contact Services Assessment, February 7, 2008
329044  
H-MA-08-01, Harris Nuclear Plant Maintenance Assessment, July 2, 2008
337027  
H-TQ-07-01, Harris Nuclear Plant Training and Qualification Assessment, May 18, 2007
234055  
216880, Maintenance Procedure Backlog and Quality, August 6-10, 2009
270275  
312544, RFO-15 Post Outage Self Assessment, May 18 - June 15, 2009
291396  
314117, Harris Mid-Cycle Assessment, January 26 - February 6, 2009
291403  
264521, Closed Systems With the Source of Demineralized Water, June 2 - 5, 2008
302656  
H-ES-09-01, Harris Engineering Support Section Assessment
306234  
H-EC-08-01, HNP Environmental and Chemistry, Assessment, April 9, 2008
H-EC-06-01, HNP Environmental and Chemistry, Assessment, April 25, 2006
Audits and Self-Assessment Items  
H-FR-07-03, Results of Environmental and Chemistry Review, January 28, 2008
07-16-SP-H, HNP Nuclear Safety Culture Assessment, June 6, 2007  
H-EP-08-01, HNP Emergency Preparedness Assessment, September 26, 2008
H-SE-06-01, Harris Site Wide Self Evaluation, June 20, 2006  
H-EP-07-01, HNP Emergency Preparedness Assessment, October 15, 2007
H-SE-08-01, Harris Nuclear Plant Self Evaluation and Human Performance Assessment,  
H-SC-08-01, HNP Security Assessment, May 29, 2008
June 16, 2008  
H-SC-07-01, HNP Security Assessment, June 14, 2007
H-OP-09-01, Assessment of Harris Operations Program, September 14, 2009  
Effectiveness Reviews
H-OM-FR-09-03, Focused Review of Return to Service Plans, January 19-23, 2009  
250171       226902       225952         222534         206710       201667
H-MC-08-01, Harris Nuclear Material and Contact Services Assessment, February 7, 2008  
Work Orders
H-MA-08-01, Harris Nuclear Plant Maintenance Assessment, July 2, 2008  
01299014     01083809     01083013       01407305       01432464     01007488
H-TQ-07-01, Harris Nuclear Plant Training and Qualification Assessment, May 18, 2007  
01301181     01536832     01116354       01172181       01154591     01432540
216880, Maintenance Procedure Backlog and Quality, August 6-10, 2009  
01557072     01579680     01581990       01581962       01503467     01120864
312544, RFO-15 Post Outage Self Assessment, May 18 - June 15, 2009  
00417204     01150648     01284574       01293105       01300467     01300968
314117, Harris Mid-Cycle Assessment, January 26 - February 6, 2009  
01346720     01346721     01363224       01396056       01396242     01496138
264521, Closed Systems With the Source of Demineralized Water, June 2 - 5, 2008  
01500794     01542758     01544206       00103940       794838       1057227
H-ES-09-01, Harris Engineering Support Section Assessment  
1062572       1137107       1463763       1457995       1548788       769595
H-EC-08-01, HNP Environmental and Chemistry, Assessment, April 9, 2008  
769599       1342247       1342249       1342251       1136753       1527115
H-EC-06-01, HNP Environmental and Chemistry, Assessment, April 25, 2006  
1527116       1402107       1076326       1070000       1133326       1379777
H-FR-07-03, Results of Environmental and Chemistry Review, January 28, 2008  
1291028       1439053       1535610       1367060       1552520
H-EP-08-01, HNP Emergency Preparedness Assessment, September 26, 2008  
Engineering Changes
H-EP-07-01, HNP Emergency Preparedness Assessment, October 15, 2007  
EC66198, Evaluation of R14 UT Results of Service Water Piping, Revision 0
H-SC-08-01, HNP Security Assessment, May 29, 2008  
H-SC-07-01, HNP Security Assessment, June 14, 2007
Effectiveness Reviews  
250171  
226902  
225952  
222534  
206710  
201667  
Work Orders  
01299014  
01083809  
01083013  
01407305  
01432464  
01007488  
01301181  
01536832  
01116354  
01172181  
01154591  
01432540  
01557072  
01579680  
01581990  
01581962  
01503467  
01120864  
00417204  
01150648  
01284574  
01293105  
01300467  
01300968  
01346720  
01346721  
01363224  
01396056  
01396242  
01496138  
01500794  
01542758  
01544206  
00103940  
794838  
1057227  
1062572  
1137107  
1463763  
1457995  
1548788  
769595  
769599  
1342247  
1342249  
1342251  
1136753  
1527115  
1527116  
1402107  
1076326  
1070000  
1133326  
1379777  
1291028  
1439053  
1535610  
1367060  
1552520  
Engineering Changes  
EC66198, Evaluation of R14 UT Results of Service Water Piping, Revision 0  
EC69988, Replace Isokinetic Sampling Skid, Revision 3
EC69988, Replace Isokinetic Sampling Skid, Revision 3
                                                                                  Attachment


                                            5
Other Documents
5  
Site Key Performance Indicators, January - August, 2009
Daily Management Review Meeting Agenda, September 15 and 16, 2009
Attachment
Joint Steering Committee and Core Team Meeting Agenda, June 2 and 4, 2009
Other Documents  
Key Performance Indicators for Site Human Performance, January - August, 2009
Site Key Performance Indicators, January - August, 2009  
Clearance Order 153137, R14 Smoke Damper Installation, October 8, 2007
Daily Management Review Meeting Agenda, September 15 and 16, 2009  
Clearance Order 108581, Replace Piston Actuator on 1MS-82, April 14, 2006
Joint Steering Committee and Core Team Meeting Agenda, June 2 and 4, 2009  
Harris Shift Narrative Log, October 8 - 19, 2007
Key Performance Indicators for Site Human Performance, January - August, 2009  
Stroke Time Trend Data for 1SW-40, 1SW-271, and 1SW-274, October 2007
Clearance Order 153137, R14 Smoke Damper Installation, October 8, 2007  
Harris Relief Request I3R-05, 2008
Clearance Order 108581, Replace Piston Actuator on 1MS-82, April 14, 2006  
Drawing 2166-B-401, Service Water System B Miscellaneous Alarms, Sheet 2232
Harris Shift Narrative Log, October 8 - 19, 2007  
Drawing 2166-B-401, Auxiliary Transfer Panel, Sheets 822, 835, 842, 847, 846, 3297
Stroke Time Trend Data for 1SW-40, 1SW-271, and 1SW-274, October 2007  
Harris Nuclear Safety Culture Assessment, June 6, 2007
Harris Relief Request I3R-05, 2008  
Harris Nuclear Safety Culture Debrief Notes, September 14-18, 2009
Drawing 2166-B-401, Service Water System B Miscellaneous Alarms, Sheet 2232  
Harris Shift Narrative Log, October 14-16, 2007
Drawing 2166-B-401, Auxiliary Transfer Panel, Sheets 822, 835, 842, 847, 846, 3297  
Calculation CT-0063, Void Size Acceptance Criteria for Presence of Air within the Containment
Harris Nuclear Safety Culture Assessment, June 6, 2007  
Spray Additive System, Revision 0
Harris Nuclear Safety Culture Debrief Notes, September 14-18, 2009  
Calculation HNP-M/Mech-1095, Limiting Void Sizes for Containment Spray Suction Piping,
Harris Shift Narrative Log, October 14-16, 2007  
        Revision 0
Calculation CT-0063, Void Size Acceptance Criteria for Presence of Air within the Containment  
Drawing CPL-2165, S-0550, Containment Spray System, Revision 16
Spray Additive System, Revision 0  
NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73, Revision 2
Calculation HNP-M/Mech-1095, Limiting Void Sizes for Containment Spray Suction Piping,  
Main Steam Isolation Valves 80, 82, and 84 Closed Stroke Time Trends, 2001-2009
Revision 0  
4085 - Essential Services Chilled Water System Health Report, July 28, 2009
Drawing CPL-2165, S-0550, Containment Spray System, Revision 16  
ESCW Preventative Maintenance for 2007, September 30, 2009
NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73, Revision 2  
3Q07 - 4Q08 Site Trend Reports, Self Evaluation Rollup and Trend Analysis
Main Steam Isolation Valves 80, 82, and 84 Closed Stroke Time Trends, 2001-2009  
Plant Nuclear Safety Committee Action Items, July 15, 2009
4085 - Essential Services Chilled Water System Health Report, July 28, 2009  
Nuclear Safety Review Committee Meeting Minutes, August 21, 2007, October 29, 2007,
ESCW Preventative Maintenance for 2007, September 30, 2009  
        June 3, 2008, August 19, 2008
3Q07 - 4Q08 Site Trend Reports, Self Evaluation Rollup and Trend Analysis  
SD-148, System Description, Essential Services Chilled Water, Revision 15
Plant Nuclear Safety Committee Action Items, July 15, 2009  
DBD-132, Design Basis Document, Essential and Nonessential Services Chilled Water,
Nuclear Safety Review Committee Meeting Minutes, August 21, 2007, October 29, 2007,  
        Revision 10
June 3, 2008, August 19, 2008  
Drawing 5-S-0998, Simplified Flow Diagram, HVAC Essential Services Chilled Water,
SD-148, System Description, Essential Services Chilled Water, Revision 15  
        Revision 7
DBD-132, Design Basis Document, Essential and Nonessential Services Chilled Water,  
CPL 2166 S-0302, Medium Voltage Relay Settings 6900V Emer. Bus 1A-SA Sheets 20, 23 and
Revision 10  
        24, Revision 9
Drawing 5-S-0998, Simplified Flow Diagram, HVAC Essential Services Chilled Water,  
SD-156, Plant Electrical Distribution System Description, Revision 13
Revision 7  
System Health Report 6.9KV AC Distribution, 1st Quarter 2009, July 20, 2009
CPL 2166 S-0302, Medium Voltage Relay Settings 6900V Emer. Bus 1A-SA Sheets 20, 23 and  
System Health Report Radiation Monitoring, 1st Quarter 2009, July 14, 2009
24, Revision 9  
Calculation E2-0005.09 Degraded Grid Voltage Protection For 6.9 kV Busses 1A-SA & 1B-SB,
SD-156, Plant Electrical Distribution System Description, Revision 13  
        Revision 2
System Health Report 6.9KV AC Distribution, 1st Quarter 2009, July 20, 2009  
CAR-SH-N-029, Safety-Related Radiation Monitoring System Specification, Revision 6
System Health Report Radiation Monitoring, 1st Quarter 2009, July 14, 2009  
System 5145 (Startup and Auxiliary Transformers) Maintenance Rule Scoping Document
Calculation E2-0005.09 Degraded Grid Voltage Protection For 6.9 kV Busses 1A-SA & 1B-SB,  
System 5165 (6.9 KV AC Distribution) Maintenance Rule Scoping Document
Revision 2  
STGP 208986 - Strategic Plan to replace 6.9kV air circuit breakers with vacuum breakers
CAR-SH-N-029, Safety-Related Radiation Monitoring System Specification, Revision 6  
        Westinghouse Technical Bulletin TB-07-5, May 14, 2007
System 5145 (Startup and Auxiliary Transformers) Maintenance Rule Scoping Document  
SD-118, Radiation Monitoring System Description, Revision 10
System 5165 (6.9 KV AC Distribution) Maintenance Rule Scoping Document  
DBD-304, Radiation Monitoring System and Gross Failed Fuel Detector Design Basis
STGP 208986 - Strategic Plan to replace 6.9kV air circuit breakers with vacuum breakers  
        Document, Revision 9
Westinghouse Technical Bulletin TB-07-5, May 14, 2007  
                                                                                    Attachment
SD-118, Radiation Monitoring System Description, Revision 10  
DBD-304, Radiation Monitoring System and Gross Failed Fuel Detector Design Basis  
Document, Revision 9


                                              6
Preventative Maintenance Requests 253955, 313698
6  
Calculation 0054-JRG, PSB-1 Loss of Offsite Power Relay Settings, Revision 3
Maintenance Rule Expert Panel meeting summary, November 15, 2007
Attachment
Harris Main Condenser Trending Basis Document
Preventative Maintenance Requests 253955, 313698  
Harris Nuclear Plant Emergency Preparedness Zone Siren Acoustic Study
Calculation 0054-JRG, PSB-1 Loss of Offsite Power Relay Settings, Revision 3  
Harris Emergency Preparedness Siren Battery Backup Power Calculations
Maintenance Rule Expert Panel meeting summary, November 15, 2007  
Areva, Shearon Harris End of Cycle 15 Fuel Inspection Results
Harris Main Condenser Trending Basis Document  
Environmental and Chemistry - Leadership Improvement Plan
Harris Nuclear Plant Emergency Preparedness Zone Siren Acoustic Study  
Environmental and Chemistry - Self Evaluation Overview
Harris Emergency Preparedness Siren Battery Backup Power Calculations  
Drawing 2165-S-0550, Simplified Flow Diagram Containment Spray System
Areva, Shearon Harris End of Cycle 15 Fuel Inspection Results  
Containment Spray System Troubleshooting Plan, September 17, 2009
Environmental and Chemistry - Leadership Improvement Plan  
Calculation CT-0027, Detail Calculation of NaOH Eductor Loop
Environmental and Chemistry - Self Evaluation Overview  
LER 2008-003-00, Manual actuation of the Reactor Protection System During Shutdown Rod
Drawing 2165-S-0550, Simplified Flow Diagram Containment Spray System  
        Position Indication Surveillance testing
Containment Spray System Troubleshooting Plan, September 17, 2009  
LER 2007-002-00, Control Rod Shutdown Bank Anomaly Causes Entry into TS 3.0.3
Calculation CT-0027, Detail Calculation of NaOH Eductor Loop  
LER 2008-002-00, Manual Actuation of the Reactor Protection System due to Main Condenser
LER 2008-003-00, Manual actuation of the Reactor Protection System During Shutdown Rod  
        Exhaust Boot Failure
Position Indication Surveillance testing  
LER 2008-001-00, Containment Spray Additive System Eductor Test Flow Outside of TS limits
LER 2007-002-00, Control Rod Shutdown Bank Anomaly Causes Entry into TS 3.0.3  
HNP Shift Narrative Log, September 17, 2009
LER 2008-002-00, Manual Actuation of the Reactor Protection System due to Main Condenser  
Steam Generator Blowdown System Training Manual, Revision 5
Exhaust Boot Failure  
9001-Containment Isolation Valve Health Report. July 23, 2009
LER 2008-001-00, Containment Spray Additive System Eductor Test Flow Outside of TS limits  
EIR 20090373, Equipment Inoperable Record 1SP-217, May 19, 2009
HNP Shift Narrative Log, September 17, 2009  
DBD-101, Reactor Coolant Sampling, Revision 5
Steam Generator Blowdown System Training Manual, Revision 5  
9001-Containment Isolation Valve Health Report. July 23, 2009  
EIR 20090373, Equipment Inoperable Record 1SP-217, May 19, 2009  
DBD-101, Reactor Coolant Sampling, Revision 5  
Operator Challenges Log, August 2009
Operator Challenges Log, August 2009
                                                                                Attachment
}}
}}

Latest revision as of 08:33, 14 January 2025

IR 05000400-09-006; 09/14/2009 - 10/02/2009; Shearon Harris Nuclear Power Plant, Unit 1; Biennial Inspection of the Identification and Resolution of Problems
ML093060038
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 10/30/2009
From: Daniel Merzke
Reactor Projects Branch 7
To: Burton C
Carolina Power & Light Co
References
IR-09-006
Download: ML093060038 (29)


See also: IR 05000400/2009006

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

SAM NUNN ATLANTA FEDERAL CENTER

61 FORSYTH STREET, SW, SUITE 23T85

ATLANTA, GEORGIA 30303-8931

October 30, 2009

Mr. Christopher L. Burton

Vice President

Carolina Power & Light Company

Shearon Harris Nuclear Plant

P.O. Box 165, Mail Zone 1

New Hill, NC 27562-0165

SUBJECT:

SHEARON HARRIS NUCLEAR POWER PLANT - NRC PROBLEM

IDENTIFICATION AND RESOLUTION INSPECTION

REPORT 05000400/2009006

Dear Mr. Burton:

On October 2, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection

at your Shearon Harris reactor facility. The enclosed report documents the inspection findings,

which were discussed on October 2, 2009, and October 26, 2009, with you and other members

of your staff.

The inspection was an examination of activities conducted under your license as they relate to

the identification and resolution of problems, compliance with the Commissions rules and

regulations, and with the conditions of your operating license. Within these areas, the

inspection involved examination of selected procedures and representative records,

observations of plant equipment and activities, and interviews with personnel.

On the basis of the samples selected for review, the team concluded that in general, problems

were properly identified, evaluated, and resolved within the problem identification and resolution

program. However, during the inspection, some examples of minor issues were identified in the

areas of identification of issues, prioritization and evaluation of issues, and effectiveness of

corrective actions. This report documents two NRC identified findings that were evaluated

under the significance determination process as having very low safety significance (Green).

These issues were determined to involve violations of NRC requirements. However, because of

their very low safety significance and because they were entered into your corrective action

program, the NRC is treating these findings as non-cited violations consistent with

Section VI.A.1 of the NRC Enforcement Policy. If you wish to contest these non-cited violations,

you should provide a response within 30 days of the date of this inspection report, with the basis

for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk,

Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director,

Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC

20555-0001; and the NRC Senior Resident Inspector at the Shearon Harris Nuclear Plant.

CP&L

2

In addition, if you disagree with the characterization of any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Shearon Harris Power Plant. The information you provide will be considered in accordance with

Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any), will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Daniel Merzke, Acting Chief

Reactor Projects Branch 7

Division of Reactor Projects

Docket Nos.

50-400

License Nos. DPR-63

Enclosure:

Inspection Report 05000400/2009006

w/Attachment: Supplemental Information

cc w/encl. (See page 3)

CP&L

2

In addition, if you disagree with the characterization of any finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Shearon Harris Power Plant. The information you provide will be considered in accordance with

Inspection Manual Chapter 0305.

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any), will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Daniel Merzke, Acting Chief

Reactor Projects Branch 7

Division of Reactor Projects

Docket Nos.

50-400

License Nos. DPR-63

Enclosure:

Inspection Report 05000400/2009006

w/Attachment: Supplemental Information

cc w/encl. (See page 3)

SUNSI Rev Compl.

Yes No

ADAMS

Yes No

Reviewer Initials

Publicly Avail

Yes No

Sensitive

Yes ; No

Sens. Type Initials

RIV:DRP

RII:DRP

RII:DRP

RII:DRS

RII:DRP

MCatts

PLessard

PNiebaum

RTaylor

EStamm

MPS4 by email PBL1 by email PKN by email

RCT1 by email EJS2

10/29/09

10/29/09

10/29/09

10/29/09

10/30/09

RII:DRP

RII:DRP

DMerzke

RMusser

DXM2

RAM

10/30/09

10/30/09

OFFICIAL RECORD COPY DOCUMENT NAME: S:\\DRP\\RPB7\\PI&R\\PI&R\\InspectionReports\\Harris PIR Inspection

Report 2009006 rev 7.doc

T=Telephone E=E-mail F=Fax

CP&L

3

cc w/encl:

Brian C. McCabe

Manager, Nuclear Regulatory Affairs

Progress Energy Carolinas, Inc.

Electronic Mail Distribution

R. J. Duncan, II

Vice President

Nuclear Operations

Carolina Power & Light Company

Electronic Mail Distribution

Greg Kilpatrick

Training Manager

Shearon Harris Nuclear Power Plant

Progress Energy Carolinas, Inc.

Electronic Mail Distribution

John Warner

Manager

Support Services

Progress Energy Carolinas, Inc.

Electronic Mail Distribution

David H. Corlett

Supervisor

Licensing/Regulatory Programs

Progress Energy

Electronic Mail Distribution

David T. Conley

Associate General Counsel

Legal Dept.

Progress Energy Service Company, LLC

Electronic Mail Distribution

Christos Kamilaris

Director

Fleet Support Services

Carolina Power & Light Company

Electronic Mail Distribution

John H. O'Neill, Jr.

Shaw, Pittman, Potts & Trowbridge

2300 N. Street, NW

Washington, DC 20037-1128

Chairman

North Carolina Utilities Commission

Electronic Mail Distribution

Beverly O. Hall

Chief, Radiation Protection Section

Department of Environmental Health

N.C. Department of Environmental

Commerce & Natural Resources

Electronic Mail Distribution

Public Service Commission

State of South Carolina

P.O. Box 11649

Columbia, SC 29211

Robert P. Gruber

Executive Director

Public Staff - NCUC

4326 Mail Service Center

Raleigh, NC 27699-4326

Herb Council

Chair

Board of County Commissioners of Wake

County

P.O. Box 550

Raleigh, NC 27602

Tommy Emerson

Chair

Board of County Commissioners of

Chatham County

186 Emerson Road

Siler City, NC 27344

Kelvin Henderson

Plant General Manager

Carolina Power and Light Company

Shearon Harris Nuclear Power Plant

Electronic Mail Distribution

cc w/encl. (continued page 4)

CP&L

4

cc w/encl. (continued)

Senior Resident Inspector

Carolina Power and Light Company

Shearon Harris Nuclear Power Plant

U.S. NRC

5421 Shearon Harris Rd

New Hill, NC 27562-9998

CP&L

5

Letter to Christopher L. Burton from Daniel Merzke dated October 30, 2009.

SUBJECT:

SHEARON HARRIS NUCLEAR POWER PLANT - NRC PROBLEM

IDENTIFICATION AND RESOLUTION INSPECTION REPORT

05000400/2009006

Distribution w/encl:

C. Evans, RII EICS

L. Slack, RII EICS

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMShearonHarris Resource

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.:

50-400

License Nos.:

DPR-63

Report No:

05000400/2009006

Licensee:

Carolina Power and Light Company (CP&L)

Facility:

Shearon Harris Nuclear Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill, NC 27562

Dates:

September 14 - 18, 2009

September 28 - October 2, 2009

Inspectors:

M. Catts, Resident Inspector, Palo Verde, Team Leader

P. Lessard, Resident Inspector, Harris

P. Niebaum, Resident Inspector, Hatch

R. Taylor, Senior Project Inspector

E. Stamm, Project Engineer

Approved by:

Daniel Merzke, Acting Chief

Reactor Projects Branch 7

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000400/2009006; 09/14/2009 - 10/02/2009; Shearon Harris Nuclear Power

Plant, Unit 1; biennial inspection of the identification and resolution of problems.

The inspection was conducted by a senior project inspector, three resident inspectors, and a

project engineer. Two Green findings of very low safety significance were identified during the

inspection. The significance of most findings is indicated by their color (Green, White, Yellow,

or Red) using Inspection Manual Chapter 0609, "Significance Determination Process." The

cross-cutting aspects were determined using Inspection Manual Chapter 0305, "Operating

Reactor Assessment Program." Findings for which the significance determination process does

not apply may be Green or be assigned a severity level after NRC management's review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

Identification and Resolution of Problems

The inspection team concluded that, in general, problems were adequately identified, prioritized,

and evaluated; and effective corrective actions were implemented. Site management was

actively involved in the corrective action program and focused appropriate attention on

significant plant issues. The team found that employees were encouraged by management to

initiate corrective action documents to address plant issues.

The licensee generally had an adequate threshold for identifying and correcting problems, as

evidenced by the relatively few deficiencies identified by the NRC that had not been previously

identified by the licensee during the review period. Action requests normally provided complete

and accurate characterization of the problem. However, the team identified a minor violation

and seven minor issues during plant walkdowns and document reviews where problems were

not identified and entered into the corrective action program by the licensee.

Generally, prioritization and evaluation of issues were adequate, consistent with the licensees

corrective action program guidance. Formal root cause evaluations for significant problems

were adequate, and corrective actions specified for problems addressed the cause of the

problems. The age and extensions for completing evaluations were closely monitored by plant

management, both for high priority nuclear condition reports, as well as for adverse conditions

of lower priority. Also, the technical adequacy and depth of evaluations (e.g., root cause

investigations) were typically adequate. However, the team identified one unresolved item and

two minor issues associated with prioritization and evaluation of issues.

Corrective actions were generally timely, commensurate with the safety significance of the

issues, and effective, in that conditions adverse to quality were corrected in accordance with the

licensee CAP procedures. For the significant conditions adverse to quality that were reviewed,

generally the corrective actions directly addressed the cause and effectively prevented

recurrence, as evidenced by a review of performance indicators, nuclear condition reports, and

discussions with licensee staff that demonstrated that the significant conditions adverse to

quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence

were scheduled consistent with licensee procedures. However, during the review of nuclear

3

Enclosure

condition reports, the team identified two violations of NRC requirements and an additional

minor issue regarding adequacy and timeliness of corrective actions.

The operating experience program was effective in screening operating experience for

applicability to the plant, entering items determined to be applicable into the corrective action

program, and taking adequate corrective actions to address the issues. External and internal

operating experience were adequately utilized and considered as part of formal root cause

evaluations for supporting the development of lessons learned and corrective actions.

The licensees audits and self-assessments were critical and effective in identifying issues and

entering them into the corrective action program. These audits and assessments identified

issues similar to those identified by the NRC with respect to the effectiveness of the corrective

action program.

Based on general discussions with licensee employees during the inspection, targeted

interviews with plant personnel, and reviews of selected employee concerns records, the team

determined that personnel at the site felt free to raise safety concerns to management and use

the corrective action program as well as the employee concerns program to resolve those

concerns.

A.

NRC Identified Findings

Cornerstone: Barrier Integrity

Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, "Corrective Action," for the licensees failure to identify the cause

and take corrective actions to preclude repetition of a significant condition

adverse to quality for both containment spray additive system eductors being

outside of the technical specification flow band. Specifically, between July 2009

and the present, the violation occurred when Eductor A was found three times

and Eductor B was found once outside of the Technical Specification 3.6.2.2 flow

band. This issue was previously identified as a significant condition adverse to

quality in January 2008, but the corrective actions taken failed to preclude

repetition. The licensee entered this issue into the corrective action program as

nuclear condition report 356873. The licensee took immediate corrective actions

to throttle the eductor flow to within the band, and is developing corrective

actions to preclude repetition.

The finding is more than minor because it is associated with the design control

attribute of the Barrier Integrity Cornerstone and affects the cornerstone objective

of providing reasonable assurance that physical design barriers, such as the

iodine scrubbing capability of the containment spray additive system eductors,

will protect the public from radionuclide releases caused by accidents or events.

Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and

Characterization of Findings," the finding was determined to have a very low

safety significance because it did not represent a degradation of the radiological

barrier function provided for the control room, auxiliary building, or spent fuel

pool; the finding did not represent a degradation of the barrier function of the

4

Enclosure

control room against smoke or a toxic atmosphere; the finding did not represent

an actual open pathway in the physical integrity of reactor containment; and the

finding did not involve an actual reduction in function of the hydrogen igniters in

the reactor containment. The finding had a cross-cutting aspect in the area of

problem identification and resolution associated with the corrective action

program because the licensee did not thoroughly evaluate problems such that

the resolutions address causes and extent of conditions, as necessary, and for

significant problems, conduct effectiveness reviews of corrective actions to

ensure that the problems are resolved (P.1(c)) (Section 4OA2.a(3)(i)).

Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion XVI, "Corrective Action," for the licensees failure to correct a condition

adverse to quality in a timely manner. Specifically, between May 27, 1997 and

September 29, 2007, Main Steam Isolation Valve 82 close stroke time exhibited

a condition adverse to quality for a trend degrading towards the technical

specification limit, without sufficient corrective actions to prevent failure. This

resulted in Main Steam Isolation Valve 82 exceeding the five-second stroke time

limit required in Technical Specification 3.7.1.5. The licensee entered this issue

into the corrective action program as nuclear condition report 358464.

This finding is more than minor because it is associated with the containment

barrier performance attribute of the Barrier Integrity Cornerstone and affects the

cornerstone objective of providing reasonable assurance that physical design

barriers, such as the main steam isolation valve radiological release barrier

required for a steam generator tube rupture, protect the public from radionuclide

releases caused by accidents or events. Using Manual Chapter 0609.04, "Phase

1 - Initial Screening and Characterization of Findings," the finding was

determined to have a very low safety significance because it did not represent a

degradation of the radiological barrier function provided for the control room,

auxiliary building, or spent fuel pool; the finding did not represent a degradation

of the barrier function of the control room against smoke or a toxic atmosphere;

the finding did not represent an actual open pathway in the physical integrity of

reactor containment; and the finding did not involve an actual reduction in

function of the hydrogen igniters in the reactor containment. This finding had a

cross-cutting aspect in the area of human performance associated with decision-

making because the licensee did not use conservative assumptions so that

safety-significant decisions were verified to validate underlying assumptions and

identify unintended consequences (H.1.(b)) (Section 4OA2.a(3)(ii)).

B.

Licensee Identified Violations

None

Enclosure

REPORT DETAILS

4.

OTHER ACTIVITIES

4OA2 Problem Identification and Resolution

a.

Assessment of the Corrective Action Program

(1)

Inspection Scope

The inspectors reviewed the licensees corrective action program (CAP) procedures

which described the administrative process for initiating and resolving problems primarily

through the use of action requests (ARs), which were then processed into the CAP as

nuclear condition reports (NCRs). The team selected and reviewed a sample of NCRs

that had been issued between August 2007 and August 2009. This period of time was

purposefully chosen to follow the last Biennial Problem Identification and Resolution

(PI&R) inspection conducted in August 2007. This review was performed to verify that

problems were being properly identified, appropriately characterized, and entered into

the CAP for resolution. Where possible, the team independently verified that the

corrective actions were implemented as intended.

Within the time frame described above, the team selected NCRs from principally four

specific areas of interest. The first inspection area consisted of a detailed review of

selected NCRs associated with four risk-significant systems: emergency AC power (non-

emergency diesel generator (EDG)), essential services chilled water, containment

isolation Target Rock valves, and low head safety injection (LHSI) / residual heat

removal (RHR) system. The team conducted plant walkdowns of equipment associated

with the selected systems and other plant areas to assess the material condition and to

look for any deficiencies that had not been previously entered into the CAP. The team

reviewed NCRs, maintenance history, completed work orders (WOs) for the systems,

and reviewed associated system health reports. These reviews were performed to verify

that problems were being properly identified, appropriately characterized, and entered

into the CAP for resolution. Items reviewed generally covered a two-year period of time;

however, in accordance with the inspection procedure, the team performed a five-year

review of age-dependent issues for containment isolation Target Rock valves and

LHSI/RHR.

The second inspection area consisted of a detailed review of a representative number of

NCRs that were assigned to the major plant departments, including operations,

maintenance, engineering, health physics, chemistry, emergency preparedness, and

security. This selection was performed to ensure that samples were reviewed across all

cornerstones of safety identified in the NRCs Reactor Oversight Process (ROP). These

NCRs were reviewed to assess each departments threshold for identifying and

documenting plant problems, thoroughness of evaluations, and adequacy of corrective

actions. The team also attended meetings where NCRs were screened for significance

Enclosure

6

to determine whether the licensee was identifying, accurately characterizing, and

entering problems into the CAP at an appropriate threshold.

For the third inspection area, the team selected a sample of NRC issued non-cited

violations and findings, licensee identified violations, and Licensee Event Reports

(LERs), to verify the effectiveness of the licensees CAP implementation regarding NRC

inspection findings and reportable events issued since the previous 2007 PI&R

inspection.

The fourth inspection area covered the review of NCRs associated with selected issues

of interest, specifically maintenance rule functional failures, non-conforming/degraded

conditions, and radiation monitors performance issues. The team reviewed the NCRs to

verify that problems were identified, evaluated, and resolved in accordance with the

licensees procedures and applicable NRC Regulations.

Among the four areas mentioned above, the team conducted a detailed review of

selected root-cause and apparent-cause evaluations of the problems identified. The

team reviewed these evaluations against the descriptions of the problem described in

the NCRs and the guidance in licensee Procedure CAP-NGGC-0205, "Significant

Adverse Condition Investigations and Adverse Condition Investigations-Increased

Rigor." The team assessed if the licensee had adequately determined the cause(s) of

identified problems, and had adequately addressed operability, reportability, common

cause, generic concerns, extent-of-condition, and extent-of-cause. The review also

assessed if the licensee had appropriately identified and prioritized corrective actions to

prevent recurrence.

Additionally, the team performed control room walkdowns to assess the main control

room (MCR) deficiency list and to ascertain if deficiencies were entered into the CAP.

Operator workarounds and operator burden screenings were reviewed, and the team

verified compensatory measures for deficient equipment which were being implemented

in the field.

Finally, the team reviewed site trend reports, to determine if the licensee effectively

trended identified issues and initiated appropriate corrective actions when adverse

trends were identified. The team attended various plant meetings to observe

management oversight and implementing functions of the corrective action process.

These included Management Review of NCRs meetings and Unit Evaluators meetings.

Documents reviewed are listed in the Attachment.

(2)

Assessment

Identification of Issues

The team determined that the licensee generally had an adequate threshold for

identifying and correcting problems as evidenced by: the relatively few deficiencies

identified by the NRC that had not been previously identified by the licensee during the

review period; the type of problems identified and corrected; the review of licensee

Enclosure

7

requirements for initiating corrective action documents as described in licensee

Procedure CAP-NGGC-0200, "Corrective Action;" the management expectation that

employees were encouraged to initiate NCRs or work orders; a review of system health

reports; and the teams observations during plant walkdowns. However, the team

identified a minor violation and seven minor issues during plant walkdowns and

document reviews where problems were not identified and entered into the CAP by the

licensee. Trending was generally effective in monitoring and identifying plant issues;

however, the team determined that not enough time had passed to assess trends or for

the licensee to develop goals and thresholds for the newly developed performance

indicators, such as corrective maintenance backlog or preventative maintenance

deferred. Site management was actively involved in the CAP and focused appropriate

attention on significant plant issues.

The team identified the following minor violation:

testing required to demonstrate that structures, systems, and components will

perform satisfactorily in service is identified and performed in accordance with

written test procedures. It further states that test results shall be documented and

evaluated to assure that test requirements have been satisfied. Contrary to the

above, on September 30, 2009, the team identified data recorded per

Procedure MST-I0412, "Waste Processing Building (WPB) Stack 5 Flow Rate

Monitor and Isokinetic Sampling System Calibration dated August 20, 2009," was

outside the allowable range and was not discovered prior to returning the WPB Vent

Stack 5 Flow Rate Monitor and the associated Wide Range Gas Monitor (WRGM) to

service. Upon discovery, the licensee declared the WRGM inoperable and initiated

appropriate compensatory actions pending a subsequent performance of calibration

Procedure MST-I0412. This failure to comply with 10 CFR Part 50, Appendix B,

Criterion XI, "Test Control," constitutes a violation of minor significance that is not

subject to enforcement action in accordance with the NRC's Enforcement Policy.

This issue is similar to NRCs Inspection Manual Chapter 0612, Appendix E,

Example 1(a), in that the data was incorrectly recorded during the procedure and

there was reasonable assurance that the Flow Stack Monitor and the associated

WRGM remained operable as evidenced by a successful retest per licensee

Procedure MST-I0412. The licensee entered this issue into the CAP as

NCR 358187.

The team identified the following minor issues:

The team identified a potential adverse trend in maintenance induced voiding of

safety-related systems. Specifically, voids had been introduced during maintenance

on an emergency service water (ESW) pump, a normal service water pump, a

containment spray pump, and an auxiliary feedwater pump. No operability issues

exist for these pumps. The licensee entered this issue into the CAP as NCR

356943.

Nuclear Condition Report 357122 was written to address refrigerant/oil leakage on

Essential Services Chiller B. Per Procedure CAP-NGGC-0200, this NCR should

Enclosure

8

have been routed to the MCR so the licensee could appropriately explore any impact

upon operability. The licensee identified that the NCR had not been properly routed

to the MCR and took corrective action. However, the licensee failed to identify that

the NCR not being properly routed to the MCR was an adverse condition. Following

discussions with the inspection team, the licensee concluded that not routing the

NCR to the MCR was an adverse condition and entered the issue into the CAP as

NCR 357595.

Emergency Diesel Generator A Frequency Transducer failed on

September 11, 2009; however, NCR 247241 was not written until nine days after the

failure. Procedure CAP-NGGC-0200 requires an NCR to be written promptly. There

was no impact to having this NCR written late. The licensee entered this issue into

the CAP as NCR 358348.

The team reviewed the MCR logs for radiation monitor failures and discovered

Channel 2 of Radiation Monitor RM-3567ASA was declared inoperable on

June 8, 2009. During troubleshooting efforts, the licensee discovered that the

Channel 2 detector had failed. The team questioned the licensee and discovered an

NCR was not initiated to document this event. Not entering this issue into CAP had

no effect on plant equipment. The licensee entered this issue into the CAP as NCR

358412.

During a walkdown of the RHR Trains A and B with the licensee, the inspector

identified multiple deficiencies which required entry into the CAP. The licensee

initiated NCR 355964 for obsolete testing devices remaining on motor operated valve

actuators. The licensee initiated NCR 355989 for both RHR pump vibration

monitoring cables not enclosed in flexible conduit as per design. The licensee

entered two other conditions into the CAP via work requests (WR): WR 399084 for

boric acid staining below 1RH-30 (RHR A Heat Exchanger Discharge Valve) and WR 399087 for boric acid on 1SI-359 (LHSI Supply Isolation Valve). Lastly, the licensee

initiated WR 399078 for a minor grease leak on 1SI-341 (RHR B Shutdown Cooling

Isolation Valve). The team determined that none of these issues impacted

operability of the RHR system.

The MCR annunciator inverter power transfer setpoints were erroneously set to

104 Vdc/Vac during replacement in July 2008. This value was below the plant

drawing and vendor recommended setpoint of 120 +/- 10% Vdc/Vac. The licensee

entered this issue into the CAP as NCR 355911, determined there was no current

impact, and initiated a compensatory measure to log inverter voltage once each shift

to assure that the setpoint deficiency had no impact on the functionality of the MCR

annunciators.

A safety system outage on ESW Train A, which caused a quantitative yellow risk

condition was extended and scheduled to overlap a qualitative yellow risk condition.

After this condition was identified, the licensee delayed the qualitative yellow risk

condition to prevent overlapping yellow risk conditions. The licensees

Procedure WCM-001, "On-Line Maintenance Risk Management," offered no

Enclosure

9

guidance to consider the combined effect of quantitative and qualitative risk

conditions. The licensee entered this issue into the CAP as NCR 356048.

Prioritization and Evaluation of Issues

Based on the review of audits conducted by the licensee and the assessment conducted

by the inspection team during the onsite period, the team concluded that problems were

generally prioritized and evaluated in accordance with the licensees CAP procedures as

described in the NCR Processing Guidelines in Procedure CAP-NGGC-0200. Each

NCR written was assigned a priority level at the NCR review meetings. Management

reviews of NCRs were thorough and adequate consideration was given to system or

component operability and associated plant risk.

The team determined that the station had conducted root cause and apparent cause

analyses in compliance with the licensees CAP procedures, and assigned cause

determinations were appropriate considering the significance of the issues being

evaluated. A variety of causal-analysis techniques were used depending on the type

and complexity of the issue consistent with licensee Procedure CAP-NGGC-0205.

The team determined that generally, the licensee had performed evaluations that were

technically accurate and of sufficient depth. The team further determined that

operability, reportability, and degraded or non-conforming condition determinations had

been completed consistent with the guidance contained in Procedures CAP-NGGC-0200

and OPS-NGGC-1305, "Operability Determinations." However, the team identified one

unresolved item (URI) which is documented in Section 4OA2.a(3)(iii) of this report, and

two minor issues in this assessment area during the review of NCRs:

Emergency Diesel Generator A Frequency Transducer failed on

September 11, 2009; however, the licensee determined a reportability review was

not required for the failed component as documented in NCR 247241.

Procedure CAP-NGGC-0200 requires NCRs be reviewed for reportability. The

licensee performed a preliminary review and determined that the frequency

transducer failed in a conservative direction. The licensee entered this issue into the

CAP as NCR 357786.

Nuclear Condition Report 263267 investigated the degraded grid time delay relays

for the safety-related 6.9 kilovolt (kV) Busses 1A-SA and 1B-SB that failed their

as-found TS surveillance test during refueling outage (RFO) 14. The team

questioned the licensee on their selected cause for the relay failures and determined

that the defective relays were not quarantined or evaluated, following their

replacement, in an effort to validate the selected cause. The licensee entered this

issue into the CAP as NCR 358290 to improve the quarantine process for defective

parts. The team concluded that the selected cause was adequate based on

available information and that corrective action to replace the failed relays with a

different type of relay was adequate.

Enclosure

10

Effectiveness of Corrective Actions

Based on a review of corrective action documents, interviews with licensee staff, and

verification of completed corrective actions, the team determined that overall, corrective

actions were timely, commensurate with the safety significance of the issues, and

effective, in that conditions adverse to quality were corrected in accordance with the

licensee CAP procedures. For the significant conditions adverse to quality reviewed,

generally the corrective actions directly addressed the cause and effectively prevented

recurrence, as evidenced by a review of performance indicators, NCRs, and discussions

with licensee staff that demonstrated that the significant conditions adverse to quality

had not recurred. Effectiveness reviews for corrective actions to preclude recurrence

(CAPRs) were scheduled consistent with licensee procedures. However, during the

review of NCRs, the team identified two violations of NRC requirements and an

additional minor issue regarding adequacy and timeliness of corrective actions.

The team identified the following two violations:

was found three times and Eductor B was found once outside of the TS 3.6.2.2 flow

band. This issue was previously identified as a significant condition adverse to

quality in January 2008, but the corrective actions taken failed to preclude

recurrence. The team identified one finding for the failure to identify the cause and

take CAPR of a significant condition adverse to quality for both containment spray

additive system eductors being outside of the TS flow band as documented in

Section 4OA2.a(3)(i). The licensee entered this issue into the CAP as NCR 356873.

Between May 27, 1997 and September 29, 2007, Main Steam Isolation Valve MS-82

close stroke time exhibited a degrading trend towards the TS limit without sufficient

corrective actions to prevent failure. This resulted in MS-82 exceeding the five-

second stroke time limit required in TS 3.7.1.5. The team identified one finding for

failure to correct a condition adverse to quality in a timely manner as documented in

Section 4OA2.a(3)(ii). The licensee entered this issue into the CAP as NCR 358464.

The team identified the following minor issue:

Nuclear Condition Report 290961 evaluated the failure of the main condenser

expansion joint that caused a loss of vacuum and resulted in a manual trip of the

unit. This issue was discussed in more detail in LER 2008-002-00. The team

determined that while the corrective actions were generally adequate, the expansion

joint inspection instructions do not contain specific acceptance criteria. Specific

acceptance criteria for inspecting for dry rot, cracking, splitting or other signs of

degradation is necessary to ensure an objective review to determine if results are

satisfactory. The team determined that the potential still exists for degradation not

being properly identified. The licensee entered this issue into the CAP as NCR

358345.

Enclosure

11

(3)

Findings

(i)

Failure to Preclude Repetition of a Significant Condition Adverse to Quality for Both

Containment Spray Additive System Eductors Being Outside of the Technical

Specification Flow Band

Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, "Corrective Action," for the licensees failure to identify the

cause and take CAPR of a significant condition adverse to quality for both containment

spray additive system eductors being outside of the TS flow band, which resulted in

Eductor A found three times and Eductor B found once outside of the TS 3.6.2.2 flow

band between July 2009 and the present.

Description. Between November 2007 and May 2008, the containment spray additive

system eductors were found outside of the TS 3.6.2.2 flow band seven times. In

January 2008, the licensee determined that this was a significant condition adverse to

quality and performed a root cause investigation. During the course of their

investigation, the licensee identified two root causes: entrapped air in the system and

inadequate system design. As CAPRs, the licensee established a procedure to identify

air voids in the system, revised the operations procedure to prevent the eductors from

being operated with the suction line isolated, and installed more stable throttle valves in

the suction line. The licensee reported the condition to the NRC in May 2008 as

LER 2008-01-00. This LER was closed as a Licensee Identified Violation (LIV) in

Inspection Report 05000400/2008004.

The purpose of the eductor is to introduce sodium hydroxide (NaOH) into the

containment spray (CT) system flow during a loss of coolant accident. If there is too little

eductor flow, not enough NaOH would be present and the iodine scrubbing capability of

the CT system would be reduced. If too much NaOH is present, CT flow pH could rise

high enough to increase degradation of aluminum in containment. This could result in

increased debris accumulating on the emergency core cooling system recirculation

sump screens and reducing performance of the emergency core cooling system. During

their previous investigation, the licensee determined that they had experienced eductor

flows both above and below the TS flow band.

The team reviewed the licensees implementation of the CAPRs, and determined the

CAPRs were ineffective at precluding repetition of a significant condition adverse to

quality since the eductor flows were discovered outside of the TS band between

July 2009 and the present. On three occasions flow was below the TS band, and on one

occasion flow was above the TS band. The licensee took immediate corrective actions

to adjust flow back into the TS band. Additionally, the licensee developed a

compensatory measure to dispatch a dedicated operator to adjust flow as necessary in

the case of CT initiation. The licensee initiated NCR 356873, reopened the root cause

investigation, is reevaluating the cause determination that was performed in 2008, and is

developing additional CAPRs to address the root cause.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to identify the cause and take CAPR of a significant condition adverse

Enclosure

12

to quality, resulting in both containment spray additive system eductors being outside of

the TS 3.6.2.2 flow band. The finding is more than minor because it is associated with

the design control attribute of the Barrier Integrity Cornerstone and affects the

cornerstone objective of providing reasonable assurance that physical design barriers,

such as the iodine scrubbing capability of the containment spray additive system

eductors, will protect the public from radionuclide releases caused by accidents or

events. Using Manual Chapter 0609.04, "Phase 1 - Initial Screening and

Characterization of Findings," the finding was determined to have a very low safety

significance because it did not represent a degradation of the radiological barrier

function provided for the control room, auxiliary building, or spent fuel pool; the finding

did not represent a degradation of the barrier function of the control room against smoke

or a toxic atmosphere; the finding did not represent an actual open pathway in the

physical integrity of reactor containment; and the finding did not involve an actual

reduction in function of the hydrogen igniters in the reactor containment. The finding has

a cross-cutting aspect in the area of problem identification and resolution associated with

the corrective action program because the licensee did not thoroughly evaluate

problems such that the resolutions address causes and extent of conditions, as

necessary, and for significant problems, conduct effectiveness reviews of corrective

actions to ensure that the problems are resolved (P.1(c)).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, "Corrective Action," requires, in part, that in the case of a significant

condition adverse to quality, the measures taken shall assure that the cause of the

condition is determined and corrective action should preclude repetition. Contrary to this

requirement, the licensee failed to identify the cause and take CAPR of both

containment spray additive system eductors being outside of the TS flow band.

Specifically, between July 2009 and the present, the violation occurred when Eductor A

was found three times and Eductor B was found once outside of the TS 3.6.2.2 flow

band.

The licensee took immediate corrective action to throttle eductor flow to within the TS

band, and is developing CAPRs. Because the finding is of very low safety significance

and has been entered into the licensees CAP as NCR 356873, this violation is being

treated as an NCV consistent with Section VI.A.1 of the Enforcement Policy:

NCV 05000400/ 2009006-01, "Failure to Preclude Repetition of a Significant Condition

Adverse to Quality for Both Containment Spray Additive System Eductors Being Outside

of the Technical Specification Flow Band."

(ii)

Failure to Correct a Condition Adverse to Quality Involving a Main Steam Isolation Valve

Degrading Trend Before Valve Failure

Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, "Corrective Action," for the licensees failure to correct a

condition adverse to quality in a timely manner, which resulted in MS-82 exceeding the

TS stroke time limit.

Description. On September 29, 2007, Valve MS-82 failed surveillance test

Procedure OST-1046, "Main Steam Isolation Valve Operability Test Quarterly Interval

Enclosure

13

Mode 3 to 5," due to exceeding the close stroke time limit of five seconds. Technical

Specification Surveillance Requirement 4.7.1.5, "Main Steam Line Isolation Valves,"

requires this valve to stroke close within five seconds. The main steam isolation valves

are required to close to act as a barrier to a radiological release during a steam

generator tube rupture or to mitigate a main steam line break. The licensee declared

Valve MS-82 inoperable, wrote NCR 248429, and performed WO 1120864 to repair the

valve and decrease the stroke time.

The licensee had been trending the close stroke time of Valve MS-82 since

December 29, 1986. The close stroke time trend started to degrade around

May 27, 1997. In May 2004, the valve was labeled low margin due to the valve stroking

close at 4.74 seconds, which was approaching the five-second limit. Between May 2004

and RFO 13 in April 2006, the valve stroke time continued to increase so that at the start

of RFO 13 the valve stroked close at 4.96 seconds. The licensee replaced the actuator

of the valve; however, the as-left valve stroke time at the end of RFO 13 was still near

the TS limit at 4.92 seconds.

The licensee developed contingency WO 1120864 for RFO 14, to gain stroke time

margin by adjusting the air operated valve hydraulic system flow control valve. During

RFO 14, on September 29, 2007, Valve MS-82 failed the stroke time close test by

stroking at 5.17 seconds. The licensee implemented contingency WO 1120864.

The team reviewed NCR 248429 and the close stroke time trend for Valve MS-82. The

team questioned why the degrading trend since 1997 had not been identified, and an

NCR had not been written to correct the condition. The team determined that unlike the

other valves in the in-service testing program, no process or procedure existed to

identify a degrading trend on a main steam isolation valve, write a NCR, and correct the

condition before valve failure. The team determined this issue was indicative of current

plant performance since no process or procedure currently exists.

The team questioned that with the degrading trend nearing the close stroke time limit,

why effective maintenance was not performed in RFO 13 to ensure the valve would not

exceed the TS close stroke time before RFO 14. The team reviewed the surveillance

test performed on April 8, 2006, and noted that the licensee was still in Mode 5 where

maintenance could have been performed on the valve. However, the team noted that

the surveillance test results were not reviewed until April 11, 2006, when the plant was in

Mode 3, when maintenance could not be performed on the valve. The team also

reviewed NCR 248429 that stated "It consistently has been a conscious decision not to

adjust these valves to gain stroke time margin because of the ensuing post maintenance

test required." This NCR also stated that the decision not to perform maintenance was

deemed to be an acceptable risk. Not performing effective maintenance on the

degrading stroke time close trend for Valve MS-82 led to the failure of this valve in

RFO 14. The licensee wrote NCR 358464 to address why corrective actions were not

taken before Valve MS-82 failed.

Analysis. The performance deficiency associated with this finding involved the

licensees failure to correct a condition adverse to quality in a timely manner, which

resulted in Valve MS-82 exceeding the TS stroke time limit. This finding is more than

Enclosure

14

minor because it is associated with the containment barrier performance attribute of the

Barrier Integrity Cornerstone and affects the cornerstone objective of providing

reasonable assurance that physical design barriers, such as the main steam isolation

valve radiological release barrier required for a steam generator tube rupture, protect

the public from radionuclide releases caused by accidents or events. Using Manual

Chapter 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," the

finding was determined to have a very low safety significance because it did not

represent a degradation of the radiological barrier function provided for the control room,

auxiliary building, or spent fuel pool; the finding did not represent a degradation of the

barrier function of the control room against smoke or a toxic atmosphere; the finding did

not represent an actual open pathway in the physical integrity of reactor containment;

and the finding did not involve an actual reduction in function of the hydrogen igniters in

the reactor containment. This finding has a cross-cutting aspect in the area of human

performance associated with decision-making because the licensee did not use

conservative assumptions so that safety-significant decisions were verified to validate

underlying assumptions and identify unintended consequences (H.1.(b)).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, "Corrective Action," requires, in part, that measures shall be established

to assure that conditions adverse to quality are promptly identified and corrected.

Contrary to this requirement, between May 27, 1997 and September 29, 2007, the

licensee failed to identify and correct a condition adverse to quality for a trend degrading

towards the technical specification limit, without sufficient corrective actions to prevent

failure. This resulted in Main Steam Isolation Valve 82 exceeding the five-second stroke

time limit required in Technical Specification 3.7.1.5. Because the finding is of very low

safety significance and has been entered into the licensees CAP as NCR 358464, this

violation is being treated as an NCV consistent with Section VI.A.1 of the Enforcement

Policy: NCV 05000400/2009006-02, "Failure to Correct a Condition Adverse to Quality

Involving a Main Steam Isolation Valve Degrading Trend Before Valve Failure."

(iii)

Unresolved Item Associated With the Evaluation of the Failure of Emergency Service

Water Valve 271

Introduction. The inspectors identified a URI associated with the evaluation of the failure

of ESW Auxiliary Reservoir Discharge Valve 271 to open on the start of ESW Pump B.

Description. On October 19, 2007, while in Mode 5, ESW Auxiliary Reservoir Discharge

Valve 271 failed to open on the start of ESW Pump B. This valve is required to open on

the start of an ESW pump to provide a discharge path for the cooling water. Operators

immediately stopped ESW Pump B and aligned normal service water to the safety

related components in Train B. The licensee determined that the auto open controls for

Valve SW-271 had been disabled by a clearance order for unrelated work. Although

ESW Train B is not required to be operational in Mode 5, the components cooled by

ESW Train B, such as EDG B and RHR Train B, were being relied upon as protected

train equipment. Therefore, ESW Train B was necessary to ensure core decay heat

removal in the event that off-site power was not available. NRC inspectors wrote a

self-revealing NCV of TS 6.8.1, "Programs and Procedures," for an inadequate

clearance order as documented in NRC Integrated Inspection Report

Enclosure

15

05000400/2007005. The team reviewed the evaluation performed for this NCV including

the reportability review. The reportability review stated this condition was not reportable

since operators were able to open this valve manually from the control room. The team

questioned whether the operators would be able to open the valve within one minute,

which is required to ensure cooling to the EDGs during an accident. The team also

determined that when the valve is manually opened by the reactor operators from the

control room, that the valve would automatically go closed due to the inadequate

clearance. As a result of the teams questions, the licensee wrote NCR 358062 and

determined that the failure of SW-271 to open was a MRFF. This failure did not exceed

the ESW Train B maintenance rule performance criteria. The licensee determined that

this failure affected the MSPI. This condition could prevent the fulfillment of the safety

function of EDG B and RHR B that are needed to maintain the reactor in a safe

shutdown condition or to remove residual heat. The licensee wrote NCR 361821 to

address this issue. This issue is considered unresolved pending additional NRC review

of the evaluation of the failure including the reportability review, the risk assessment, and

the corrective actions: URI 05000400/2009006-03, "Unresolved Item Associated with

the Evaluation of the Failure of Emergency Service Water Valve 271."

b.

Assessment of the Use of Operating Experience

(1)

Inspection Scope

The team examined licensee programs for reviewing industry operating experience

(OE), reviewed licensees Procedure CAP-NGGC-0202, "Operating Experience

Program," and reviewed the licensees OE database, to assess the effectiveness of how

external and internal OE data was handled at the plant. In addition, the team selected

OE documents (e.g., NRC generic communications, 10 CFR Part 21 reports, LERs,

vendor notifications, etc.), which had been issued since August 2007, to verify whether

the licensee had appropriately evaluated each notification for applicability to the Shearon

Harris Nuclear Power Plant, and whether issues identified through these reviews were

entered into the CAP.

Documents reviewed are listed in the Attachment.

(2)

Assessment

Based on interviews and a review of documentation related to the review of OE issues,

the team determined that the licensee was generally effective in screening OE for

applicability to the plant. Industry OE was evaluated at either the corporate or plant level

depending on the source and type of document. Relevant information was then

forwarded to the applicable department for further action or informational purposes.

Operating experience issues requiring action were entered into the CAP for tracking and

closure. In addition, OE was included in apparent cause and root cause evaluations in

accordance with licensee Procedure CAP-NGGC-0205.

(3)

Findings

No findings of significance were identified.

Enclosure

16

c.

Assessment of Self-Assessments and Audits

(1)

Inspection Scope

The team reviewed audit reports and self-assessment reports, including those which

focused on problem identification and resolution, to assess the thoroughness and

self-criticism of the licensee's audits and self-assessments, and to verify that problems

identified through those activities were appropriately prioritized and entered into the CAP

for resolution in accordance with licensee Procedure CAP-NGGC-0201,

"Self-Assessment and Benchmark Programs."

(2)

Assessment

The team determined that the scopes of assessments and audits were adequate.

Self-assessments were generally detailed and critical, as evidenced by findings

consistent with the teams independent review. Self-assessment findings related to

issues or weaknesses were entered into the CAP and tracked to completion based on

the NCR priority level. Corrective actions for self-assessment findings were adequate to

address the issues. Generally, the licensee performed evaluations that were technically

accurate. Site trend reports were thorough and a low threshold was established for

evaluation of potential trends; however, the team determined that not enough time had

passed to assess trends or for the licensee to develop goals and thresholds for the

newly developed performance indicators, such as corrective maintenance backlog or

preventative maintenance deferred. The team concluded that the self-assessments and

audits were an effective tool to identify adverse trends.

(3)

Findings

No findings of significance were identified.

d.

Assessment of Safety-Conscious Work Environment

(1)

Inspection Scope

The team randomly interviewed 29 on-site workers from maintenance, security,

operations, chemistry, and engineering organizations regarding their knowledge of the

corrective action program at Shearon Harris and their willingness to write NCRs or raise

safety concerns. During technical discussions with members of the plant staff, the team

conducted interviews to develop a general perspective of the safety-conscious work

environment at the site. The interviews were also conducted to determine if any

conditions existed that would cause employees to be reluctant to raise safety concerns.

The team reviewed the licensees employee concerns program (ECP) and interviewed

the ECP coordinator. Additionally, the team reviewed the latest Safety Culture

Assessment to evaluate the thoroughness and self-criticism of the licensee's

assessment, and to verify that problems identified were appropriately prioritized and

entered into the CAP for resolution. Finally, the team reviewed a sample of completed

ECP reports to verify that concerns were being properly reviewed and identified

deficiencies were being resolved and entered into the CAP when appropriate.

Enclosure

17

(2)

Assessment

Based on the interviews conducted and the NCRs reviewed, the team determined that

licensee management emphasized the need for all employees to identify and report

problems using the appropriate methods established within the administrative programs,

including the CAP and ECP. These methods were readily accessible to all employees.

Based on discussions conducted with a sample of plant employees from various

departments, the team determined that employees felt free to raise issues, and that

management encouraged employees to place issues into the CAP for resolution. The

team did not identify any reluctance on the part of the licensee staff to report safety

concerns.

(3)

Findings

No findings of significance were identified.

4OA6 Meetings, Including Exit

On October 2, 2009, the team presented the inspection results to Mr. Christopher Burton

and other members of the site staff. On October 26, 2009, the team lead re-exited the

inspection results concerning the unresolved item to Mr. Dave Corlett.

The team confirmed that all proprietary information reviewed was returned to the

licensee during the inspection.

ATTACHMENT: SUPPPLEMENTAL INFORMATION

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

B. Bernard, Superintendent, Security

C. Burton, Vice President Harris Plant

D. Corlett, Supervisor, Licensing/Regulatory Programs

J. Dills, Manager, Operations

J. Doorhy, Licensing

K. Harshaw, Manager, Outage and Scheduling

K. Henderson, Plant General Manager

J. Jankens, Supervisor, Radiation Control

G. Kilpatrick, Training Manager

P. Morales, Employee Concerns Program

L. Morgan, Supervisor, Self Evaluation Unit

S. OConnor, Manager, Engineering

M. Parker, Superintendent, Radiation Protection

B. Parks, Manager, Nuclear Oversight Section

J. Robinson, Superintendent, Environmental and Chemistry

H. Szews, CAP Coordinator

J. Warner, Manager, Support Services

NRC

J. Austin, Senior Resident Inspector

R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects, Region II

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed 05000400/2009006-01

NCV

Failure to Preclude Repetition of a Significant

Condition Adverse to Quality for Both Containment

Spray Additive System Eductors Being Outside of the

Technical Specification Flow Band (Section

4OA2.a(3)(i))05000400/2009006-02

NCV

Failure to Correct a Condition Adverse to Quality

Involving a Main Steam Isolation Valve Degrading

Trend Before Valve Failure (Section 4OA2.a(3)(ii))

Opened 05000400/2009006-03

URI

Unresolved Item Associated with the Evaluation of the

Failure of Emergency Service Water Valve 271

(Section 4OA2.a(3)(iii))

Closed

None

Discussed

None

Attachment

LIST OF DOCUMENTS REVIEWED

Procedures

ADM-NGGC-0113, Performance Planning and Monitoring, Revision 0

ADM-NGGC-0101, Maintenance Rule Program, Revision 20

ADM-NGGC-0104, Work Management Process, Revision 33

AP-013, Plant Nuclear Safety Committee, Revision 34

AP-930, Plant Observation Program, Revision 10

AOP-022, Loss of Service Water, Revision 29

OPS-NGGC-1305 Operability Determinations, Revision 1

CAP-NGGC-0200, Corrective Action Program, Revision 27

CAP-NGGC-0201, Self Assessment and Benchmark Programs, Revision 12

CAP-NGGC-0202, Operating Experience Program, Revision 15

CAP-NGGC-0205, Significant Adverse Condition Investigations and Adverse Condition

Investigations - Increased Rigor, Revision 9

CAP-NGGC-0206, Corrective Action Program Trending and Analysis, Revision 3

NOS-NGGC-0400, Employee Concerns Program, Revision 0

EGR-NGGC-0010, System & Component Trending Program and System Notebooks,

Revision 13

ISI-801, Inservice Testing of Valves, Revision 47

HESS Standards, Revision 5

OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,

Revision 12

PLP-624, Mechanical Equipment Qualification Program, Revision 18

OP-148, Essential Services Chilled Water System, Revisions 37 and 49

HPS-NGGC-0003, Radiological Posting, Labeling and Surveys, Revision 14

MST-E0045, 6.9 KV Emergency Bus 1A-SA and 1B-SB Under Voltage Relay Channel

Calibration, Revision 23

ADM-NGCC-0203, Preventative Maintenance and Surveillance Testing Administration,

Revision 13

OST-1124, Train B 6.9 KV Emergency Bus Undervoltage Trip Actuating Device Operational

Test and Contact Check Modes 1-6, Revision 25

HPS-NGGC-1000, Radiation Protection and Conduct of Operations, Revision 0

SP-013 Administrative/Support Key and Lock Control, Revision 12

AP-504 Administrative Controls for Locked and Very High Radiation Areas, Revision 29

PLP-511 Radiation Control and Protection Program, Revision 20

CRC-240 Plant Vent Stack 1 Effluent Sampling, Revision 11

HNPS-NGGC-0003, Radiological Posting, Labeling and Surveys, Revision 14

MST-E0075, 6.9 KV Emergency Buses, 1A-SA and 1B-SB Undervoltage (Loss of Voltage)

Channel Calibration, Revision 6

NGGM-IA-0038, Carolinas - Nuclear Generation Group Siren Maintenance, Revision 1

ERC-004, Environmental and Chemistry Administrative Guidelines, Revision 25

SEC-NGGC-2120, Protection of Safeguards Information, Revision 22

WCM-001, On-Line Maintenance Risk Management, Revision 20

OST-1118, Containment Spray Operability Train A Quarterly Interval Modes 1-4, Revision 33

OST-1119, Containment Spray Operability Train B Quarterly Interval Modes 1-4, Revision 35

MST-I0019, Main Steam/Feedwater Flow Loop 2 Channel Calibration, Revision 16

ADM-NGGC-0104, Work Management Process, Revision 33

MMM-002, Corrective Maintenance, Revision 17

3

Attachment

MNT-NGGC-1000, Fleet Conduct of Maintenance, Revision 0

WCM-005, Work Order Prioritization Process, Revision 8

Completed Surveillance Tests

OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,

Revision 12, September 29, 2007

OST-1046, Main Steam Isolation Valve Operability Test Quarterly Interval Mode 3 to 5,

Revision 12, May 11, 2006

MST-I0412, Waste Processing Building (WPB) Stack 5 Flow Rate Monitor and Isokinetic

Sampling System Calibration, August 20, 2009

Action Requests/Nuclear Condition Reports

223911

244705

245320

245633

246582

247241

248429

250575

250810

262037

263421

266234

269409

279287

279715

281217

286843

297210

300052

300163

301267

315670

318483

320236

320444

323631

329044

330455

337027

338184

340240

340325

230031

238372

238374

263439

263441

270215

282037

287726

249284

330423

301267

329438

331701

346484

282037

279704

358062

350078

251296

249347

357786

250810

279715

244705

249347

344729

266234

248429

249992

253347

257853

262001

262192

263486

265063

267065

267066

267080

267244

268566

269406

271452

275878

278486

280015

281538

285149

285222

290761

299832

306876

316594

319422

333716

196258

221803

222730

224208

228947

253347

314660

301267

300163

286843

280649

279988

277165

269409

251296

249347

266234

263921

250810

248429

247241

244705

246582

262037

245320

245633

281217

330455

279715

231046

303142

211360

246397

292892

332141

334996

246397

292892

334934

334167

334937

263267

334936

249331

316381

253376

245663

286104

288188

326920

310739

226843

267946

307600

340516

329378

352310

283579

274978

255529

330676

241895

261182

231941

328537

201481

229805

248378

226843

327372

301730

315269

171602

188528

191359

197522

207516

223563

225187

236248

243993

246188

247129

251191

252290

254402

258053

258053

261182

263759

270318

274708

279681

281080

291651

292337

305661

313305

323057

331371

349905

350640

351437

351623

351623

355964

355989

244576

248430

252234

252471

264812

302079

317205

317280

329488

329489

331169

333828

333830

336394

340319

310373

336342

336569

247193

251437

266063

278730

279326

4

Attachment

297789

Operating Experience Action Requests

306876

317361

327306

297210

329044

337027

234055

270275

291396

291403

302656

306234

Audits and Self-Assessment Items

07-16-SP-H, HNP Nuclear Safety Culture Assessment, June 6, 2007

H-SE-06-01, Harris Site Wide Self Evaluation, June 20, 2006

H-SE-08-01, Harris Nuclear Plant Self Evaluation and Human Performance Assessment,

June 16, 2008

H-OP-09-01, Assessment of Harris Operations Program, September 14, 2009

H-OM-FR-09-03, Focused Review of Return to Service Plans, January 19-23, 2009

H-MC-08-01, Harris Nuclear Material and Contact Services Assessment, February 7, 2008

H-MA-08-01, Harris Nuclear Plant Maintenance Assessment, July 2, 2008

H-TQ-07-01, Harris Nuclear Plant Training and Qualification Assessment, May 18, 2007

216880, Maintenance Procedure Backlog and Quality, August 6-10, 2009

312544, RFO-15 Post Outage Self Assessment, May 18 - June 15, 2009

314117, Harris Mid-Cycle Assessment, January 26 - February 6, 2009

264521, Closed Systems With the Source of Demineralized Water, June 2 - 5, 2008

H-ES-09-01, Harris Engineering Support Section Assessment

H-EC-08-01, HNP Environmental and Chemistry, Assessment, April 9, 2008

H-EC-06-01, HNP Environmental and Chemistry, Assessment, April 25, 2006

H-FR-07-03, Results of Environmental and Chemistry Review, January 28, 2008

H-EP-08-01, HNP Emergency Preparedness Assessment, September 26, 2008

H-EP-07-01, HNP Emergency Preparedness Assessment, October 15, 2007

H-SC-08-01, HNP Security Assessment, May 29, 2008

H-SC-07-01, HNP Security Assessment, June 14, 2007

Effectiveness Reviews

250171

226902

225952

222534

206710

201667

Work Orders

01299014

01083809

01083013

01407305

01432464

01007488

01301181

01536832

01116354

01172181

01154591

01432540

01557072

01579680

01581990

01581962

01503467

01120864

00417204

01150648

01284574

01293105

01300467

01300968

01346720

01346721

01363224

01396056

01396242

01496138

01500794

01542758

01544206

00103940

794838

1057227

1062572

1137107

1463763

1457995

1548788

769595

769599

1342247

1342249

1342251

1136753

1527115

1527116

1402107

1076326

1070000

1133326

1379777

1291028

1439053

1535610

1367060

1552520

Engineering Changes

EC66198, Evaluation of R14 UT Results of Service Water Piping, Revision 0

EC69988, Replace Isokinetic Sampling Skid, Revision 3

5

Attachment

Other Documents

Site Key Performance Indicators, January - August, 2009

Daily Management Review Meeting Agenda, September 15 and 16, 2009

Joint Steering Committee and Core Team Meeting Agenda, June 2 and 4, 2009

Key Performance Indicators for Site Human Performance, January - August, 2009

Clearance Order 153137, R14 Smoke Damper Installation, October 8, 2007

Clearance Order 108581, Replace Piston Actuator on 1MS-82, April 14, 2006

Harris Shift Narrative Log, October 8 - 19, 2007

Stroke Time Trend Data for 1SW-40, 1SW-271, and 1SW-274, October 2007

Harris Relief Request I3R-05, 2008

Drawing 2166-B-401, Service Water System B Miscellaneous Alarms, Sheet 2232

Drawing 2166-B-401, Auxiliary Transfer Panel, Sheets 822, 835, 842, 847, 846, 3297

Harris Nuclear Safety Culture Assessment, June 6, 2007

Harris Nuclear Safety Culture Debrief Notes, September 14-18, 2009

Harris Shift Narrative Log, October 14-16, 2007

Calculation CT-0063, Void Size Acceptance Criteria for Presence of Air within the Containment

Spray Additive System, Revision 0

Calculation HNP-M/Mech-1095, Limiting Void Sizes for Containment Spray Suction Piping,

Revision 0

Drawing CPL-2165, S-0550, Containment Spray System, Revision 16

NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73, Revision 2

Main Steam Isolation Valves 80, 82, and 84 Closed Stroke Time Trends, 2001-2009

4085 - Essential Services Chilled Water System Health Report, July 28, 2009

ESCW Preventative Maintenance for 2007, September 30, 2009

3Q07 - 4Q08 Site Trend Reports, Self Evaluation Rollup and Trend Analysis

Plant Nuclear Safety Committee Action Items, July 15, 2009

Nuclear Safety Review Committee Meeting Minutes, August 21, 2007, October 29, 2007,

June 3, 2008, August 19, 2008

SD-148, System Description, Essential Services Chilled Water, Revision 15

DBD-132, Design Basis Document, Essential and Nonessential Services Chilled Water,

Revision 10

Drawing 5-S-0998, Simplified Flow Diagram, HVAC Essential Services Chilled Water,

Revision 7

CPL 2166 S-0302, Medium Voltage Relay Settings 6900V Emer. Bus 1A-SA Sheets 20, 23 and

24, Revision 9

SD-156, Plant Electrical Distribution System Description, Revision 13

System Health Report 6.9KV AC Distribution, 1st Quarter 2009, July 20, 2009

System Health Report Radiation Monitoring, 1st Quarter 2009, July 14, 2009

Calculation E2-0005.09 Degraded Grid Voltage Protection For 6.9 kV Busses 1A-SA & 1B-SB,

Revision 2

CAR-SH-N-029, Safety-Related Radiation Monitoring System Specification, Revision 6

System 5145 (Startup and Auxiliary Transformers) Maintenance Rule Scoping Document

System 5165 (6.9 KV AC Distribution) Maintenance Rule Scoping Document

STGP 208986 - Strategic Plan to replace 6.9kV air circuit breakers with vacuum breakers

Westinghouse Technical Bulletin TB-07-5, May 14, 2007

SD-118, Radiation Monitoring System Description, Revision 10

DBD-304, Radiation Monitoring System and Gross Failed Fuel Detector Design Basis

Document, Revision 9

6

Attachment

Preventative Maintenance Requests 253955, 313698

Calculation 0054-JRG, PSB-1 Loss of Offsite Power Relay Settings, Revision 3

Maintenance Rule Expert Panel meeting summary, November 15, 2007

Harris Main Condenser Trending Basis Document

Harris Nuclear Plant Emergency Preparedness Zone Siren Acoustic Study

Harris Emergency Preparedness Siren Battery Backup Power Calculations

Areva, Shearon Harris End of Cycle 15 Fuel Inspection Results

Environmental and Chemistry - Leadership Improvement Plan

Environmental and Chemistry - Self Evaluation Overview

Drawing 2165-S-0550, Simplified Flow Diagram Containment Spray System

Containment Spray System Troubleshooting Plan, September 17, 2009

Calculation CT-0027, Detail Calculation of NaOH Eductor Loop

LER 2008-003-00, Manual actuation of the Reactor Protection System During Shutdown Rod

Position Indication Surveillance testing

LER 2007-002-00, Control Rod Shutdown Bank Anomaly Causes Entry into TS 3.0.3

LER 2008-002-00, Manual Actuation of the Reactor Protection System due to Main Condenser

Exhaust Boot Failure

LER 2008-001-00, Containment Spray Additive System Eductor Test Flow Outside of TS limits

HNP Shift Narrative Log, September 17, 2009

Steam Generator Blowdown System Training Manual, Revision 5

9001-Containment Isolation Valve Health Report. July 23, 2009

EIR 20090373, Equipment Inoperable Record 1SP-217, May 19, 2009

DBD-101, Reactor Coolant Sampling, Revision 5

Operator Challenges Log, August 2009