ML111300462: Difference between revisions

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| number = ML111300462
| number = ML111300462
| issue date = 05/10/2011
| issue date = 05/10/2011
| title = IR 05000416-11-002; on 01/21/2011 03/27/2011; Grand Gulf Nuclear Station, Integrated Resident and Regional Report; Fire Protection, Maintenance Effectiveness, Radiological Hazard Assessment and Exposure Controls, and Event Follow-Up
| title = IR 05000416-11-002; on 01/21/2011 03/27/2011; Grand Gulf Nuclear Station, Integrated Resident and Regional Report; Fire Protection, Maintenance Effectiveness, Radiological Hazard Assessment and Exposure Controls, and Event Follow-Up
| author name = Gaddy V
| author name = Gaddy V
| author affiliation = NRC/RGN-IV/DRP/RPB-C
| author affiliation = NRC/RGN-IV/DRP/RPB-C
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:May 10, 2011  
                                NUCLEAR REGULATORY COMMISSION
Mr. Mike Perito  
                                                  REGI ON I V
Vice President Operations  
                                        612 EAST LAMAR BLVD, SUITE 400
Entergy Operations, Inc.  
                                        ARLINGTON, TEXAS 76011-4125
Grand Gulf Nuclear Station  
                                                May 10, 2011
P.O. Box 756  
Mr. Mike Perito
Port Gibson, MS 39150
Vice President Operations
Entergy Operations, Inc.
Grand Gulf Nuclear Station
Subject: GRAND GULF NRC INTEGRATED INSPECTION REPORT NUMBER  
P.O. Box 756
05000416/2011002  
Port Gibson, MS 39150
Subject: GRAND GULF NRC INTEGRATED INSPECTION REPORT NUMBER
Dear Mr. Perito:
          05000416/2011002
Dear Mr. Perito:
On March 27, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection  
On March 27, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection
at your Grand Gulf Nuclear Station. The enclosed integrated inspection report documents the  
at your Grand Gulf Nuclear Station. The enclosed integrated inspection report documents the
inspection findings, which were discussed on April 14, 2011, with Mike Perito, Vice President  
inspection findings, which were discussed on April 14, 2011, with Mike Perito, Vice President
Operations, and other members of your staff.
Operations, and other members of your staff.
The inspections examined activities conducted under your license as they relate to safety and
The inspections examined activities conducted under your license as they relate to safety and  
compliance with the Commissions rules and regulations and with the conditions of your license.
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
personnel.
personnel.
Based on the results of this inspection, the NRC has determined that one Severity Level IV
violation of NRC requirements occurred. The NRC has also identified five issues that were
Based on the results of this inspection, the NRC has determined that one Severity Level IV  
evaluated under the risk significance determination process as having very low safety
violation of NRC requirements occurred. The NRC has also identified five issues that were  
significance (Green). The NRC has determined that four of these findings have violations
evaluated under the risk significance determination process as having very low safety  
associated with these issues. Additionally, one licensee-identified violation, which was
significance (Green). The NRC has determined that four of these findings have violations  
determined to be of very low safety significance, is listed in this report. However, because of
associated with these issues. Additionally, one licensee-identified violation, which was  
their very low safety significance and because they were entered into your corrective action
determined to be of very low safety significance, is listed in this report. However, because of  
program, the NRC is treating these findings as noncited violations, consistent with Section 2.3.2
their very low safety significance and because they were entered into your corrective action  
of the NRC Enforcement Policy.
program, the NRC is treating these findings as noncited violations, consistent with Section 2.3.2  
If you contest the significance of the noncited violations, you should provide a response within
of the NRC Enforcement Policy.  
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with
If you contest the significance of the noncited violations, you should provide a response within  
copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV,
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of
Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with  
Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the
copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV,
NRC Resident Inspector at the facility. In addition, if you disagree with the cross-cutting aspect
612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of  
assigned to any finding in this report, you should provide a response within 30 days of the date
Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the  
NRC Resident Inspector at the facility. In addition, if you disagree with the cross-cutting aspect  
assigned to any finding in this report, you should provide a response within 30 days of the date  
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION IV
612 EAST LAMAR BLVD, SUITE 400
ARLINGTON, TEXAS 76011-4125


Entergy Operations, Inc.                     -2-
Entergy Operations, Inc.  
of this inspection report, with the basis for your disagreement, to the Regional Administrator,
- 2 -  
Region IV, and the NRC Resident Inspector at the facility.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
of this inspection report, with the basis for your disagreement, to the Regional Administrator,  
enclosures, and your response, if you choose to provide one, will be made available
Region IV, and the NRC Resident Inspector at the facility.  
electronically for public inspection in the NRC Public Document Room or from the NRC's
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
enclosures, and your response, if you choose to provide one, will be made available  
electronically for public inspection in the NRC Public Document Room or from the NRC's  
document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-
document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-
rm/adams.html. To the extent possible, your response should not include any personal privacy
rm/adams.html. To the extent possible, your response should not include any personal privacy  
or proprietary, information so that it can be made available to the Public without redaction.
or proprietary, information so that it can be made available to the Public without redaction.  
                                                Sincerely,
                                                /RA/
                                                Vincent Gaddy, Chief
Sincerely,  
                                                Project Branch C
/RA/  
                                                Division of Reactor Projects
Vincent Gaddy, Chief  
Docket: 50-416
Project Branch C  
License: NPF-29
Division of Reactor Projects  
Enclosed: NRC Inspection Report 05000416/2011002
w/Attachment: Supplemental Information
Docket:   50-416  
Distribution via ListServe
License: NPF-29  
Enclosed: NRC Inspection Report 05000416/2011002  
w/Attachment: Supplemental Information  
Distribution via ListServe  


Entergy Operations, Inc.                   -3-
Entergy Operations, Inc.  
Electronic distribution by RIV:
- 3 -  
Regional Administrator (Elmo.Collins@nrc.gov)
Deputy Regional Administrator (Art.Howell@nrc.gov)
DRP Director (Kriss.Kennedy@nrc.gov)
Electronic distribution by RIV:  
DRP Deputy Director (Troy.Pruett@nrc.gov)
Regional Administrator (Elmo.Collins@nrc.gov)  
DRS Director (Anton.Vegel@nrc.gov)
Deputy Regional Administrator (Art.Howell@nrc.gov)  
Senior Resident Inspector (Rich.Smith@nrc.gov)
DRP Director (Kriss.Kennedy@nrc.gov)  
Branch Chief, DRP/C (Vincent.Gaddy@nrc.gov)
DRP Deputy Director (Troy.Pruett@nrc.gov)  
Senior Project Engineer, DRP/C (Bob.Hagar@nrc.gov)
DRS Director (Anton.Vegel@nrc.gov)  
Project Engineer, DRP/C (Rayomand.Kumana@nrc.gov)
Senior Resident Inspector (Rich.Smith@nrc.gov)  
GG Administrative Assistant (Alley.Farrell@nrc.gov)
Branch Chief, DRP/C (Vincent.Gaddy@nrc.gov)  
Public Affairs Officer (Victor.Dricks@nrc.gov)
Senior Project Engineer, DRP/C (Bob.Hagar@nrc.gov)  
Public Affairs Officer (Lara.Uselding@nrc.gov)
Project Engineer, DRP/C (Rayomand.Kumana@nrc.gov)  
Project Manager (Alan.Wang@nrc.gov)
GG Administrative Assistant (Alley.Farrell@nrc.gov)  
Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)  
RITS Coordinator (Marisa.Herrera@nrc.gov)
Public Affairs Officer (Lara.Uselding@nrc.gov)  
Regional Counsel (Karla.Fuller@nrc.gov)
Project Manager (Alan.Wang@nrc.gov)  
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)  
RIV OEDO/ETA (Stephanie Bush-Goddard@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)  
OEMail Resource
Regional Counsel (Karla.Fuller@nrc.gov)  
ROP Reports
Congressional Affairs Officer (Jenny.Weil@nrc.gov)  
File located: R:\_REACTORS\_GG\GG 2011002 RP-RLS-vgg.docx
RIV OEDO/ETA (Stephanie Bush-Goddard@nrc.gov)  
SUNSI Rev Compl.  Yes  No ADAMS                   Yes  No     Reviewer Initials   VGG
OEMail Resource  
Publicly Avail           Yes  No Sensitive       Yes  No     Sens. Type Initials VGG
ROP Reports  
SRI:DRP/PBC                               SPE:DRP/PBC     C:DRS/EB1         C:DRS/EB2
  RLSmith                                  BHagar         TRFarnholtz       NFOKeefe
/RA/RCHagar for                           /RA/           /RA/             /RA/
5/4/2011                                 5/4/2011       4/21/2011         4/15/2011
C:DRS/OB               C:TSS             C:DRS/PSB1     C:DRS/PSB2       C:ACES/SAC
File located: R:\\_REACTORS\\_GG\\GG 2011002 RP-RLS-vgg.docx  
MHaire                 MHay             MPShannon       GEWerner         NTaylor
SUNSI Rev Compl.  
/RA/                   /RA/             /RA/           /RA/             /RA/
  Yes  No  
4/15/2011               4/18/2011         4/18/2011       4/15/2011         4/18/2011
ADAMS  
C:DRP/C
Yes  No  
  VGaddy
Reviewer Initials  
  /RA/
VGG  
  5/10/11
Publicly Avail  
OFFICIAL RECORD COPY                                   T=Telephone       E=E-mail     F=Fax
Yes  No  
Sensitive  
Yes  No  
Sens. Type Initials  
VGG  
SRI:DRP/PBC  
SPE:DRP/PBC  
C:DRS/EB1  
C:DRS/EB2  
RLSmith
   
BHagar  
TRFarnholtz  
NFOKeefe  
/RA/RCHagar for  
/RA/  
/RA/  
/RA/  
5/4/2011  
5/4/2011  
4/21/2011  
4/15/2011  
C:DRS/OB  
C:TSS  
C:DRS/PSB1  
C:DRS/PSB2  
C:ACES/SAC  
MHaire  
MHay  
MPShannon  
GEWerner  
NTaylor  
/RA/  
/RA/  
/RA/  
/RA/  
/RA/  
4/15/2011  
4/18/2011  
4/18/2011  
4/15/2011  
4/18/2011  
C:DRP/C  
   
VGaddy  
   
/RA/  
   
5/10/11  
OFFICIAL RECORD COPY
T=Telephone           E=E-mail       F=Fax  


                  U.S. NUCLEAR REGULATORY COMMISSION
                                    REGION IV
Docket:     05000416
- 1 -
License:     NPF-29
Enclosure
Report:     05000416/2011002
U.S. NUCLEAR REGULATORY COMMISSION  
Licensee:   Entergy Operations, Inc.
REGION IV  
Facility:   Grand Gulf Nuclear Station
Docket:  
Location:   7003 Baldhill Road
05000416  
            Port Gibson, MS 39150
License:  
Dates:       January 21, 2011, through March 27, 2011
NPF-29  
Inspectors: R. Smith, Senior Resident Inspector
Report:  
            M. Baquera, Resident Inspector, Palo Verde
05000416/2011002  
            A. Fairbanks, Reactor Inspector
Licensee:  
            C. Graves, Health Physicist
Entergy Operations, Inc.  
            L. Ricketson, P.E., Senior Health Physicist
Facility:  
            E. Uribe, Reactor Inspector
Grand Gulf Nuclear Station  
Approved By: Vincent Gaddy, Chief, Project Branch C
Location:  
            Division of Reactor Projects
7003 Baldhill Road  
                                    -1-                  Enclosure
Port Gibson, MS 39150  
Dates:  
January 21, 2011, through March 27, 2011  
Inspectors:  
R. Smith, Senior Resident Inspector  
M. Baquera, Resident Inspector, Palo Verde  
A. Fairbanks, Reactor Inspector  
C. Graves, Health Physicist  
L. Ricketson, P.E., Senior Health Physicist  
E. Uribe, Reactor Inspector  
Approved By:  
Vincent Gaddy, Chief, Project Branch C  
Division of Reactor Projects  


                                      SUMMARY OF FINDINGS
IR 05000416/2011002; 1/1/2011 - 3/27/2011; Grand Gulf Nuclear Station, Integrated Resident
and Regional Report; Fire Protection, Maintenance Effectiveness, Radiological Hazard
- 2 -
Assessment and Exposure Controls, and Event Follow-Up.
Enclosure
The report covered a 3-month period of inspection by resident inspectors and an announced
SUMMARY OF FINDINGS  
baseline inspection by region-based inspectors. Five Green noncited violations of significance
were identified and one Green finding of significance was identified. The significance of most
IR 05000416/2011002; 1/1/2011 - 3/27/2011; Grand Gulf Nuclear Station, Integrated Resident  
findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual
and Regional Report; Fire Protection, Maintenance Effectiveness, Radiological Hazard  
Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined
Assessment and Exposure Controls, and Event Follow-Up.  
using Inspection Manual Chapter 0310, Components Within the Cross Cutting Areas. Findings
for which the significance determination process does not apply may be Green or be assigned a
The report covered a 3-month period of inspection by resident inspectors and an announced  
severity level after NRC management review. The NRC's program for overseeing the safe
baseline inspection by region-based inspectors. Five Green noncited violations of significance  
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor
were identified and one Green finding of significance was identified. The significance of most  
Oversight Process, Revision 4, dated December 2006.
findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual  
A.     NRC-Identified Findings and Self-Revealing Findings
Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined  
        Cornerstone: Mitigating Systems
using Inspection Manual Chapter 0310, Components Within the Cross Cutting Areas. Findings  
        *       SLIV. Inspectors identified a noncited violation of 10 CFR 50.71(e)(4), which
for which the significance determination process does not apply may be Green or be assigned a  
                requires the final safety analysis report be updated, at intervals not exceeding 24
severity level after NRC management review. The NRC's program for overseeing the safe  
                months, to reflect changes made in the facility or procedures described in the
operation of commercial nuclear power reactors is described in NUREG-1649, Reactor  
                final safety analysis report. Licensee personnel failed to update the original
Oversight Process, Revision 4, dated December 2006.  
                revision of the final safety analysis report to reflect the actual number of low
                pressure coolant injection loops available for automatic initiation during shutdown
A.  
                cooling operations in Mode 3. The licensee plans to update the final safety
NRC-Identified Findings and Self-Revealing Findings  
                analysis report at the next scheduled revision. This finding was entered into the
                licensees corrective action program as condition report CR-GGN-2011-01631.
Cornerstone: Mitigating Systems  
                The failure of licensing personnel to update the final safety analysis report to
                reflect the available low pressure coolant injection loops for automatic initiation
*  
                during shutdown cooling operations in Mode 3 was a performance deficiency.
SLIV. Inspectors identified a noncited violation of 10 CFR 50.71(e)(4), which  
                This finding was evaluated using traditional enforcement because it had the
requires the final safety analysis report be updated, at intervals not exceeding 24  
                potential for impacting the NRCs ability to perform its regulatory function. The
months, to reflect changes made in the facility or procedures described in the  
                inspectors used the NRC Enforcement Policy, dated September 30, 2010, to
final safety analysis report. Licensee personnel failed to update the original  
                evaluate the significance of this violation. Consistent with the NRC Enforcement
revision of the final safety analysis report to reflect the actual number of low  
                Policy, this finding was determined to be a Severity Level IV noncited violation.
pressure coolant injection loops available for automatic initiation during shutdown  
        *       Green. The inspectors identified a noncited violation of 10 CFR Part 50.65(a)(2)
cooling operations in Mode 3. The licensee plans to update the final safety  
                for the licensees failure to demonstrate that the performance of the train B
analysis report at the next scheduled revision.   This finding was entered into the  
                control room air conditioner was being effectively controlled through the
licensees corrective action program as condition report CR-GGN-2011-01631.  
                performance of appropriate preventive maintenance. Engineering did not
The failure of licensing personnel to update the final safety analysis report to  
                properly evaluate maintenance rule functional failures resulting in the system
reflect the available low pressure coolant injection loops for automatic initiation  
                remaining in an a(2) status instead of an a(1) status. As corrective action, the
during shutdown cooling operations in Mode 3 was a performance deficiency.
                                                -2-                                  Enclosure
This finding was evaluated using traditional enforcement because it had the  
potential for impacting the NRCs ability to perform its regulatory function. The  
inspectors used the NRC Enforcement Policy, dated September 30, 2010, to  
evaluate the significance of this violation. Consistent with the NRC Enforcement  
Policy, this finding was determined to be a Severity Level IV noncited violation.  
*  
Green. The inspectors identified a noncited violation of 10 CFR Part 50.65(a)(2)  
for the licensees failure to demonstrate that the performance of the train B  
control room air conditioner was being effectively controlled through the  
performance of appropriate preventive maintenance. Engineering did not  
properly evaluate maintenance rule functional failures resulting in the system  
remaining in an a(2) status instead of an a(1) status. As corrective action, the  


  train B control room air conditioner was moved into an a(1) status. The licensee
  entered this issue into their corrective action program as Condition Report
  CR-GGN-2011-01623.
- 3 -
  The finding was more than minor because it was associated with the equipment
Enclosure
  performance attribute of the Mitigating Systems Cornerstone and adversely
train B control room air conditioner was moved into an a(1) status. The licensee  
  affected the cornerstone objective to ensure the availability, reliability, and
entered this issue into their corrective action program as Condition Report
  capability of systems that respond to initiating events to prevent undesirable
CR-GGN-2011-01623.  
  consequences. Inspectors performed a Phase 1 screening, in accordance with
  Inspection Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and
The finding was more than minor because it was associated with the equipment  
  Characterization of Findings, and determined that the finding was of very low
performance attribute of the Mitigating Systems Cornerstone and adversely  
  safety significance (Green) because the maintenance rule aspect of the finding
affected the cornerstone objective to ensure the availability, reliability, and  
  did not cause an actual loss of safety function of the system nor did it cause a
capability of systems that respond to initiating events to prevent undesirable  
  component to be inoperable. As corrective action, the train B control room air
consequences. Inspectors performed a Phase 1 screening, in accordance with  
  conditioner was moved into an (a)(1) status. This finding had a crosscutting
Inspection Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and  
  aspect in the area of human performance associated with the decision making
Characterization of Findings, and determined that the finding was of very low  
  component because licensee personnel failed to make appropriate safety-
safety significance (Green) because the maintenance rule aspect of the finding  
  significant or risk-significant decisions to address the multiple failures of the train
did not cause an actual loss of safety function of the system nor did it cause a  
  B control room air conditioner compressor. [H.1(a)] (Section 1R12.b.2)
component to be inoperable. As corrective action, the train B control room air  
* Green. The inspectors reviewed a self-revealing noncited violation of 10 CFR
conditioner was moved into an (a)(1) status. This finding had a crosscutting  
  Part 50, Appendix B, Criterion XVI, Corrective Action, after the licensee failed to
aspect in the area of human performance associated with the decision making  
  determine the cause and prevent recurrence of a significant condition adverse to
component because licensee personnel failed to make appropriate safety-
  quality associated with the train B control room air conditioner compressor
significant or risk-significant decisions to address the multiple failures of the train  
  tripping due to low oil pressure. Specifically, on December 13, 2010, the train B
B control room air conditioner compressor. [H.1(a)] (Section 1R12.b.2)  
  control room air conditioner compressor tripped on low oil pressure after the
  licensee had performed a root cause analysis to identify the cause and prevent
*  
  recurrence of a similar compressor trip on October 14, 2010. As immediate
Green. The inspectors reviewed a self-revealing noncited violation of 10 CFR  
  corrective action, the licensee installed an inline suction filter. No additional
Part 50, Appendix B, Criterion XVI, Corrective Action, after the licensee failed to  
  failures have occurred since its installation. The finding was entered into the
determine the cause and prevent recurrence of a significant condition adverse to  
  licensees corrective action program as Condition Report CR-GGN-2010-07315.
quality associated with the train B control room air conditioner compressor  
  This finding was more than minor because it was associated with the equipment
tripping due to low oil pressure. Specifically, on December 13, 2010, the train B  
  performance attribute of the Mitigating Systems Cornerstone and adversely
control room air conditioner compressor tripped on low oil pressure after the  
  affected the cornerstone objective to ensure the availability, reliability, and
licensee had performed a root cause analysis to identify the cause and prevent  
  capability of systems that respond to initiating events to prevent undesirable
recurrence of a similar compressor trip on October 14, 2010. As immediate  
  consequences. Using Inspection Manual Chapter 0609, "Significance
corrective action, the licensee installed an inline suction filter. No additional  
  Determination Process," Phase 1 worksheets, the inspectors determined that a
failures have occurred since its installation. The finding was entered into the  
  Phase 2 analysis was required because the finding represented a loss of system
licensees corrective action program as Condition Report CR-GGN-2010-07315.  
  safety function. The plant-specific risk informed notebook does not include the
This finding was more than minor because it was associated with the equipment  
  evaluation of risk caused by the loss of cooling to the main control room.
performance attribute of the Mitigating Systems Cornerstone and adversely  
  Therefore, the senior reactor analyst conducted a Phase 3 analysis. Based on
affected the cornerstone objective to ensure the availability, reliability, and  
  the bounding analysis, the analyst determined that the change in core damage
capability of systems that respond to initiating events to prevent undesirable  
  frequency result was 5.9 x 10-7. This noncited violation was therefore determined
consequences. Using Inspection Manual Chapter 0609, "Significance  
  to be of very low safety significance (Green). This finding had a crosscutting
Determination Process," Phase 1 worksheets, the inspectors determined that a  
  aspect in the area of problem identification and resolution associated with the
Phase 2 analysis was required because the finding represented a loss of system  
  corrective action program component because licensee personnel failed to
safety function. The plant-specific risk informed notebook does not include the  
                                -3-                                  Enclosure
evaluation of risk caused by the loss of cooling to the main control room.
Therefore, the senior reactor analyst conducted a Phase 3 analysis. Based on  
the bounding analysis, the analyst determined that the change in core damage  
frequency result was 5.9 x 10-7. This noncited violation was therefore determined  
to be of very low safety significance (Green). This finding had a crosscutting  
aspect in the area of problem identification and resolution associated with the  
corrective action program component because licensee personnel failed to  


      thoroughly evaluate the multiple failures of the train B control room air conditioner
      compressor. [P.1(c)] (Section 4OA3.1.b)
Cornerstone: Barrier Integrity
- 4 -
*     Green. The inspectors identified a noncited violation of Facility Operating License
Enclosure
      Condition 2.C(41), involving the failure to ensure that transient combustible were
thoroughly evaluate the multiple failures of the train B control room air conditioner  
      not stored in the fire exclusion zone near the independent spent fuel storage
compressor. [P.1(c)] (Section 4OA3.1.b)  
      installation. The inspectors performed a quarterly fire protection inspection of
      independent spent fuel storage installation and identified a large air conditioner
Cornerstone: Barrier Integrity  
      with combustible material covering it located in the fire exclusion zone that was
      within 60 feet of the dry fuel storage pad. The inspectors determined through
*  
      interviews that the material had been placed there the previous day by the
Green
      maintenance department. As immediate corrective action the licensee removed
      the combustible material from the area. The finding was entered into the
. The inspectors identified a noncited violation of Facility Operating License  
      licensees corrective action program as Condition Report CR-GGN-2011-00455.
Condition 2.C(41), involving the failure to ensure that transient combustible were  
      This finding was more than minor because it was associated human performance
not stored in the fire exclusion zone near the independent spent fuel storage  
      attribute of the Barrier Integrity Cornerstone to provide reasonable assurance
installation. The inspectors performed a quarterly fire protection inspection of  
      that physical design barriers protect the public from radionuclide releases caused
independent spent fuel storage installation and identified a large air conditioner  
      by accidents or events. Using Manual Chapter 0609, Appendix F, Fire
with combustible material covering it located in the fire exclusion zone that was  
      Protection Significance Determination Process, the inspectors determined that
within 60 feet of the dry fuel storage pad. The inspectors determined through  
      the finding impacted the fire prevention and administrative controls category.
interviews that the material had been placed there the previous day by the  
      The inspectors assigned a low degradation rating due to the fact that the amount
maintenance department. As immediate corrective action the licensee removed  
      of combustible material in the area was minimal. The inspectors concluded that
the combustible material from the area. The finding was entered into the  
      the finding was of very low safety significance (Green) due to the fact there were
licensees corrective action program as Condition Report CR-GGN-2011-00455.  
      no fire ignition sources in the area. The cause of this finding has a crosscutting
This finding was more than minor because it was associated human performance  
      aspect in the area of human performance associated with the work practices
attribute of the Barrier Integrity Cornerstone to provide reasonable assurance  
      component because the licensee failed to effectively communicate expectations
that physical design barriers protect the public from radionuclide releases caused  
      regarding storage of combustible material near the dry fuel storage pad. [H.4(b)]
by accidents or events. Using Manual Chapter 0609, Appendix F, Fire  
      (Section 1R05.1.b)
Protection Significance Determination Process, the inspectors determined that  
*     Green. The inspectors reviewed a self-revealing, Green finding of EN-DC-115,
the finding impacted the fire prevention and administrative controls category.
      Engineering Change Process, involving the failure to maintain adequate design
The inspectors assigned a low degradation rating due to the fact that the amount  
      control measures associated with the installation of the mitigation monitoring
of combustible material in the area was minimal. The inspectors concluded that  
      system. On November 8, 2010, a reactor coolant pressure boundary failure
the finding was of very low safety significance (Green) due to the fact there were  
      occurred at the skid mounted Online Noble Chemical - Mitigation Monitoring
no fire ignition sources in the area. The cause of this finding has a crosscutting  
      System pump inside primary containment. The positive displacement sample
aspect in the area of human performance associated with the work practices  
      pump ejected the pump piston from the housing, resulting in an approximate
component because the licensee failed to effectively communicate expectations  
      7 gpm leak of reactor coolant. The steam leak resulted in a reactor recirculation
regarding storage of combustible material near the dry fuel storage pad. [H.4(b)]
      system flow control valve lockup (due to hydraulic power unit motor failure) and
(Section 1R05.1.b)  
      approximately 15,000 square feet of contaminated area in the primary
      containment structure. The licensee failed to ensure proper validation testing for
*  
      the pump prior to installation. Specifically, the licensee did not ensure that the
Green. The inspectors reviewed a self-revealing, Green finding of EN-DC-115,  
      pump could withstand the operating pressures and temperatures of the system in
Engineering Change Process, involving the failure to maintain adequate design  
                                    -4-                                  Enclosure
control measures associated with the installation of the mitigation monitoring  
system. On November 8, 2010, a reactor coolant pressure boundary failure  
occurred at the skid mounted Online Noble Chemical - Mitigation Monitoring  
System pump inside primary containment. The positive displacement sample  
pump ejected the pump piston from the housing, resulting in an approximate
7 gpm leak of reactor coolant. The steam leak resulted in a reactor recirculation  
system flow control valve lockup (due to hydraulic power unit motor failure) and  
approximately 15,000 square feet of contaminated area in the primary  
containment structure. The licensee failed to ensure proper validation testing for  
the pump prior to installation. Specifically, the licensee did not ensure that the  
pump could withstand the operating pressures and temperatures of the system in  


          which it was installed. The licensee removed the mitigation monitoring system
          from service and isolated the skid from the reactor water cleanup system. This
          finding was entered into the licensees corrective action program as Condition
- 5 -
          Report CR-GGN-2010-07852.
Enclosure
          The finding is more than minor because it affects the design control attribute of
which it was installed. The licensee removed the mitigation monitoring system  
          the Barrier Integrity Cornerstone to provide reasonable assurance that physical
from service and isolated the skid from the reactor water cleanup system. This  
          design barriers protect the public from radionuclide releases caused by accidents
finding was entered into the licensees corrective action program as Condition  
          or events. Therefore, using inspection Manual Chapter 0609, "Significance
Report CR-GGN-2010-07852.  
          Determination Process," Phase 1 Worksheet for LOCA initiators, the inspectors
The finding is more than minor because it affects the design control attribute of  
          concluded that the finding was of very low safety significance (Green) because
the Barrier Integrity Cornerstone to provide reasonable assurance that physical  
          the failure of the mitigation monitoring system would not have exceeded technical
design barriers protect the public from radionuclide releases caused by accidents  
          specifications limits for identified leakage in the reactor coolant system. This
or events. Therefore, using inspection Manual Chapter 0609, "Significance  
          finding has a crosscutting aspect in the work practices component of the human
Determination Process," Phase 1 Worksheet for LOCA initiators, the inspectors  
          performance area; because the licensee failed to adequately oversee the design
concluded that the finding was of very low safety significance (Green) because  
          of the mitigation monitoring system such that nuclear safety is supported. [H.4(c)]
the failure of the mitigation monitoring system would not have exceeded technical  
          (Section 4OA3.2.b)
specifications limits for identified leakage in the reactor coolant system. This  
  Cornerstone: Occupational Radiation Safety
finding has a crosscutting aspect in the work practices component of the human  
  *       Green. The inspectors identified a noncited violation of Technical Specification
performance area; because the licensee failed to adequately oversee the design  
          5.7.2, resulting from the licensees failure to use a qualified radiation protection
of the mitigation monitoring system such that nuclear safety is supported. [H.4(c)]  
          technician to provide direct continuous coverage of work in a locked high
(Section 4OA3.2.b)  
          radiation area. The finding was placed into the corrective action program as
Cornerstone: Occupational Radiation Safety  
          Condition Report CR-GGN-2011-01045, and corrective action was being
          evaluated.
*  
          The failure to use a qualified radiation protection technician to provide direct
Green. The inspectors identified a noncited violation of Technical Specification  
          continuous coverage of work in a locked high radiation area is a performance
5.7.2, resulting from the licensees failure to use a qualified radiation protection  
          deficiency. The finding was more than minor because it was associated with the
technician to provide direct continuous coverage of work in a locked high  
          Occupational Radiation Safety Cornerstone attribute (exposure control) of
radiation area. The finding was placed into the corrective action program as  
          program and process and affected the cornerstone objective, in that, the failure
Condition Report CR-GGN-2011-01045, and corrective action was being  
          to use qualified radiation protection technicians to provide job coverage in a high
evaluated.  
          radiation area with dose rates in excess of 1000 mrem/hr had the potential to
          increase personnel dose. Using the Occupational Radiation Safety Significance
The failure to use a qualified radiation protection technician to provide direct  
          Determination Process, the inspectors determined the finding to have very low
continuous coverage of work in a locked high radiation area is a performance  
          safety significance because: (1) it was not associated with ALARA planning or
deficiency. The finding was more than minor because it was associated with the  
          work controls, (2) there was no overexposure, (3) there was no substantial
Occupational Radiation Safety Cornerstone attribute (exposure control) of  
          potential for an overexposure, and (4) the ability to assess dose was not
program and process and affected the cornerstone objective, in that, the failure  
          compromised. (Section 2RS01.b)
to use qualified radiation protection technicians to provide job coverage in a high  
B. Licensee-Identified Violations
radiation area with dose rates in excess of 1000 mrem/hr had the potential to  
  Violations of very low safety significance, which were identified by the licensee, have
increase personnel dose. Using the Occupational Radiation Safety Significance  
  been reviewed by the inspectors. Corrective actions taken or planned by the licensee
Determination Process, the inspectors determined the finding to have very low  
  have been entered into the licensees corrective action program. These violations and
safety significance because: (1) it was not associated with ALARA planning or  
  corrective action tracking numbers (condition report numbers) are listed in
work controls, (2) there was no overexposure, (3) there was no substantial  
  Section 4OA7.
potential for an overexposure, and (4) the ability to assess dose was not  
                                        -5-                                    Enclosure
compromised. (Section 2RS01.b)  
B.  
Licensee-Identified Violations  
Violations of very low safety significance, which were identified by the licensee, have  
been reviewed by the inspectors. Corrective actions taken or planned by the licensee  
have been entered into the licensees corrective action program. These violations and  
corrective action tracking numbers (condition report numbers) are listed in  
Section 4OA7.  


                                        REPORT DETAILS
Summary of Plant Status
Grand Gulf Nuclear Station began the inspection period at full rated thermal power. On January
- 6 -
9, 2011, operators reduced power to 68 percent for a planned control rod sequence exchange
Enclosure
and isolation of the moisture separator reheaters (MSRs) second stage steam to both the A
REPORT DETAILS  
and B MSRs due to tube leaks in the A MSR. The plant was returned to 96 percent power on
January 10, 2011, which was maximum power level allowed with MSR second stage steam
Summary of Plant Status
isolated. On February 18, 2011, operators reduced power to 77 percent for monthly control rod
testing, turbine testing, and to remove B heater drain pump from service in an attempt to repair
Grand Gulf Nuclear Station began the inspection period at full rated thermal power. On January  
a steam leak on the heater drain pump B discharge flange. The plant was returned to 96
9, 2011, operators reduced power to 68 percent for a planned control rod sequence exchange  
percent power on February 19, 2011. On March 11, 2011, operators reduced power to 84
and isolation of the moisture separator reheaters (MSRs) second stage steam to both the A  
percent power for a planned control rod testing and to remove B heater drain pump from
and B MSRs due to tube leaks in the A MSR. The plant was returned to 96 percent power on  
service in another attempt to repair a steam leak on the heater drain pump B discharge flange.
January 10, 2011, which was maximum power level allowed with MSR second stage steam  
The plant was returned to 96 percent power on March 12, 2011. On March 23, 2011, operators
isolated. On February 18, 2011, operators reduced power to 77 percent for monthly control rod  
reduced power to 93 percent power to remove the B heater drain pump from service again in
testing, turbine testing, and to remove B heater drain pump from service in an attempt to repair  
another attempt to repair a steam leak on the heater drain pump B pump discharge flange.
a steam leak on the heater drain pump B discharge flange. The plant was returned to 96  
The plant was returned to 96 percent power on March 12, 2011. The plant remained at 96
percent power on February 19, 2011. On March 11, 2011, operators reduced power to 84  
percent power for the remainder of the inspection period.
percent power for a planned control rod testing and to remove B heater drain pump from  
1.     REACTOR SAFETY
service in another attempt to repair a steam leak on the heater drain pump B discharge flange.
        Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and
The plant was returned to 96 percent power on March 12, 2011. On March 23, 2011, operators  
        Emergency Preparedness
reduced power to 93 percent power to remove the B heater drain pump from service again in  
1R01 Adverse Weather Protection (71111.01)
another attempt to repair a steam leak on the heater drain pump B pump discharge flange.
.1     Readiness for Seasonal Extreme Weather Conditions
The plant was returned to 96 percent power on March 12, 2011. The plant remained at 96  
  a.   Inspection Scope
percent power for the remainder of the inspection period.  
        The inspectors performed a review of the adverse weather procedures for seasonal
        extreme low temperatures. The inspectors verified that weather-related equipment
1.  
        deficiencies identified during the previous year were corrected prior to the onset of
REACTOR SAFETY  
        seasonal extremes, and evaluated the implementation of the adverse weather
        preparation procedures and compensatory measures for the affected conditions before
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and  
        the onset of, and during, the adverse weather conditions.
Emergency Preparedness  
        During the inspection, the inspectors focused on plant-specific design features and the
        procedures used by plant personnel to mitigate or respond to adverse weather
1R01 Adverse Weather Protection (71111.01)  
        conditions. Additionally, the inspectors reviewed the updated final safety analysis report
.1  
        and performance requirements for systems selected for inspection and verified that
Readiness for Seasonal Extreme Weather Conditions  
        operator actions were appropriate as specified by plant-specific procedures. Specific
a.  
        documents reviewed during this inspection are listed in the attachment. The inspectors
The inspectors performed a review of the adverse weather procedures for seasonal  
        also reviewed corrective action program items to verify that plant personnel were
extreme low temperatures. The inspectors verified that weather-related equipment  
        identifying adverse weather issues at an appropriate threshold and entering them into
deficiencies identified during the previous year were corrected prior to the onset of  
                                            -6-                                  Enclosure
seasonal extremes, and evaluated the implementation of the adverse weather  
preparation procedures and compensatory measures for the affected conditions before  
the onset of, and during, the adverse weather conditions.  
Inspection Scope
During the inspection, the inspectors focused on plant-specific design features and the  
procedures used by plant personnel to mitigate or respond to adverse weather  
conditions. Additionally, the inspectors reviewed the updated final safety analysis report  
and performance requirements for systems selected for inspection and verified that  
operator actions were appropriate as specified by plant-specific procedures. Specific  
documents reviewed during this inspection are listed in the attachment. The inspectors  
also reviewed corrective action program items to verify that plant personnel were  
identifying adverse weather issues at an appropriate threshold and entering them into  


      their corrective action program in accordance with station corrective action procedures.
      The inspectors reviews focused specifically on the following plant systems:
      *       Standby service water
- 7 -
      *       Emergency diesel generators
Enclosure
      *       Plant service water
their corrective action program in accordance with station corrective action procedures.
      *       Fire water pumps and tanks
The inspectors reviews focused specifically on the following plant systems:  
      These activities constitute completion of one readiness for seasonal adverse weather
      sample as defined in Inspection Procedure 71111.01-05.
*  
  b. Findings
Standby service water  
      No findings were identified.
*  
.2   Readiness for Impending Adverse Weather Conditions
Emergency diesel generators  
  a. Inspection Scope
*  
      Since extreme cold conditions and icing were forecast in the vicinity of the facility for
Plant service water  
      January 9, 2011, the inspectors reviewed overall preparations/protection for the
*  
      expected weather conditions. On January 7, 2011, the inspectors inspected the standby
Fire water pumps and tanks  
      service water towers because their safety-related functions could be affected as a result
      of the extreme cold and icing conditions forecast for the facility. The inspectors observed
These activities constitute completion of one readiness for seasonal adverse weather  
      space heater operation and weatherized enclosures to ensure operability of affected
sample as defined in Inspection Procedure 71111.01-05.  
      systems. The inspectors reviewed licensee procedures and discussed potential
      compensatory measures with control room personnel. The inspectors focused on plant
b.  
      managements actions for implementing the stations procedures for ensuring adequate
No findings were identified.  
      personnel for safe plant operation and emergency response would be available.
Findings
      Specific documents reviewed during this inspection are listed in the attachment.
      These activities constitute completion of one readiness for impending adverse weather
.2  
      condition sample as defined in Inspection Procedure 71111.01-05.
Readiness for Impending Adverse Weather Conditions  
  b. Findings
a.  
      No findings were identified.
Since extreme cold conditions and icing were forecast in the vicinity of the facility for  
1R04 Equipment Alignments (71111.04)
January 9, 2011, the inspectors reviewed overall preparations/protection for the  
.1   Partial Walkdown
expected weather conditions. On January 7, 2011, the inspectors inspected the standby  
  a. Inspection Scope
service water towers because their safety-related functions could be affected as a result  
      The inspectors performed partial system walkdowns of the following risk-significant
of the extreme cold and icing conditions forecast for the facility. The inspectors observed  
      systems:
space heater operation and weatherized enclosures to ensure operability of affected  
      *       Division II standby service water system during Division I maintenance outage
systems. The inspectors reviewed licensee procedures and discussed potential  
                                          -7-                                  Enclosure
compensatory measures with control room personnel. The inspectors focused on plant  
managements actions for implementing the stations procedures for ensuring adequate  
personnel for safe plant operation and emergency response would be available.
Specific documents reviewed during this inspection are listed in the attachment.  
Inspection Scope
These activities constitute completion of one readiness for impending adverse weather  
condition sample as defined in Inspection Procedure 71111.01-05.  
b.  
No findings were identified.  
Findings
1R04 Equipment Alignments (71111.04)  
.1  
Partial Walkdown  
a.  
The inspectors performed partial system walkdowns of the following risk-significant  
systems:  
Inspection Scope
*  
Division II standby service water system during Division I maintenance outage  


    *       Residual heat removal system B during residual heat removal system A
            maintenance outage
    *       Residual heat removal system C during residual heat removal system A
- 8 -
            maintenance outage
Enclosure
    *       Division II standby diesel generator system during Division I maintenance outage
*  
    *       Standby liquid control system A during standby liquid control system B
Residual heat removal system B during residual heat removal system A  
            maintenance outage
maintenance outage  
    The inspectors selected these systems based on their risk significance relative to the
    reactor safety cornerstones at the time they were inspected. The inspectors attempted
*  
    to identify any discrepancies that could affect the function of the system, and, therefore,
Residual heat removal system C during residual heat removal system A  
    potentially increase risk. The inspectors reviewed applicable operating procedures,
maintenance outage  
    system diagrams, UFSAR, technical specification requirements, administrative technical
    specifications, outstanding work orders, condition reports, and the impact of ongoing
*  
    work activities on redundant trains of equipment in order to identify conditions that could
Division II standby diesel generator system during Division I maintenance outage  
    have rendered the systems incapable of performing their intended functions. The
    inspectors also inspected accessible portions of the systems to verify system
*  
    components and support equipment were aligned correctly and operable. The
Standby liquid control system A during standby liquid control system B  
    inspectors examined the material condition of the components and observed operating
maintenance outage  
    parameters of equipment to verify that there were no obvious deficiencies. The
    inspectors also verified that the licensee had properly identified and resolved equipment
The inspectors selected these systems based on their risk significance relative to the  
    alignment problems that could cause initiating events or impact the capability of
reactor safety cornerstones at the time they were inspected. The inspectors attempted  
    mitigating systems or barriers and entered them into the corrective action program with
to identify any discrepancies that could affect the function of the system, and, therefore,  
    the appropriate significance characterization. Specific documents reviewed during this
potentially increase risk. The inspectors reviewed applicable operating procedures,  
    inspection are listed in the attachment.
system diagrams, UFSAR, technical specification requirements, administrative technical  
    These activities constitute completion of five partial system walkdown samples as
specifications, outstanding work orders, condition reports, and the impact of ongoing  
    defined in Inspection Procedure 71111.04-05.
work activities on redundant trains of equipment in order to identify conditions that could  
  b. Findings
have rendered the systems incapable of performing their intended functions. The  
    No findings were identified.
inspectors also inspected accessible portions of the systems to verify system  
1R05 Fire Protection (71111.05)
components and support equipment were aligned correctly and operable. The  
    Quarterly Fire Inspection Tours
inspectors examined the material condition of the components and observed operating  
  a. Inspection Scope
parameters of equipment to verify that there were no obvious deficiencies. The  
    The inspectors conducted fire protection walkdowns that were focused on availability,
inspectors also verified that the licensee had properly identified and resolved equipment  
    accessibility, and the condition of firefighting equipment in the following risk-significant
alignment problems that could cause initiating events or impact the capability of  
    plant areas:
mitigating systems or barriers and entered them into the corrective action program with  
    *       Division II diesel generator room (1D303)
the appropriate significance characterization. Specific documents reviewed during this  
                                          -8-                                  Enclosure
inspection are listed in the attachment.  
These activities constitute completion of five partial system walkdown samples as  
defined in Inspection Procedure 71111.04-05.  
b.  
No findings were identified.  
Findings
1R05 Fire Protection (71111.05)  
Quarterly Fire Inspection Tours  
a.  
The inspectors conducted fire protection walkdowns that were focused on availability,  
accessibility, and the condition of firefighting equipment in the following risk-significant  
plant areas:  
Inspection Scope
*  
Division II diesel generator room (1D303)  


  *       Residual heat removal pump and heat exchanger rooms A (1A102 and 1A103)
  *       Residual heat removal pump and heat exchanger rooms B (1A105 and 1A106)
  *       Reactor Core Isolation Pump Room (1A104)
- 9 -
  *       Dry fuel storage pad area (Area 59 the Yard)
Enclosure
  The inspectors reviewed areas to assess if licensee personnel had implemented a fire
*  
  protection program that adequately controlled combustibles and ignition sources within
Residual heat removal pump and heat exchanger rooms A (1A102 and 1A103)  
  the plant; effectively maintained fire detection and suppression capability; maintained
*  
  passive fire protection features in good material condition; and had implemented
Residual heat removal pump and heat exchanger rooms B (1A105 and 1A106)  
  adequate compensatory measures for out of service, degraded or inoperable fire
*  
  protection equipment, systems, or features, in accordance with the licensees fire plan.
Reactor Core Isolation Pump Room (1A104)  
  The inspectors selected fire areas based on their overall contribution to internal fire risk
*  
  as documented in the plants Individual Plant Examination of External Events with later
Dry fuel storage pad area (Area 59 the Yard)  
  additional insights, their potential to affect equipment that could initiate or mitigate a
  plant transient, or their impact on the plants ability to respond to a security event. Using
The inspectors reviewed areas to assess if licensee personnel had implemented a fire  
  the documents listed in the attachment, the inspectors verified that fire hoses and
protection program that adequately controlled combustibles and ignition sources within  
  extinguishers were in their designated locations and available for immediate use; that
the plant; effectively maintained fire detection and suppression capability; maintained  
  fire detectors and sprinklers were unobstructed; that transient material loading was
passive fire protection features in good material condition; and had implemented  
  within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
adequate compensatory measures for out of service, degraded or inoperable fire  
  be in satisfactory condition. The inspectors also verified that minor issues identified
protection equipment, systems, or features, in accordance with the licensees fire plan.
  during the inspection were entered into the licensees corrective action program.
The inspectors selected fire areas based on their overall contribution to internal fire risk  
  Specific documents reviewed during this inspection are listed in the attachment.
as documented in the plants Individual Plant Examination of External Events with later  
  These activities constitute completion of five quarterly fire-protection inspection samples
additional insights, their potential to affect equipment that could initiate or mitigate a  
  as defined in Inspection Procedure 71111.05-05.
plant transient, or their impact on the plants ability to respond to a security event. Using  
b. Findings
the documents listed in the attachment, the inspectors verified that fire hoses and  
  Introduction. The inspectors identified a Green noncited violation of Facility Operating
extinguishers were in their designated locations and available for immediate use; that  
  License Condition 2.C(41), involving the failure to ensure that transient combustible were
fire detectors and sprinklers were unobstructed; that transient material loading was  
  not stored in the fire exclusion zone near the independent spent fuel storage installation.
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to  
  Description. On January 24, 2011, the inspectors performed a quarterly fire protection
be in satisfactory condition. The inspectors also verified that minor issues identified  
  inspection of independent spent fuel storage installation. The inspectors identified a
during the inspection were entered into the licensees corrective action program.
  large air conditioner with combustible material covering it located in the fire exclusion
Specific documents reviewed during this inspection are listed in the attachment.  
  zone that appeared to be within 60 feet of the dry fuel storage pad. The inspectors
  brought this to the attention of the work center senior reactor operator. The work center
These activities constitute completion of five quarterly fire-protection inspection samples  
  senior reactor operator contacted the site fire engineer, who walked down the fire
as defined in Inspection Procedure 71111.05-05.  
  exclusion zone and determined that the combustible material covering the air conditioner
  was within the 60 feet of the dry fuel storage pad, which is in violation of plant procedural
b.  
  requirements. The inspectors determined through interviews that the material had been
Findings  
  placed there the day before by the maintenance department. The site had the air
Introduction
  conditioner and the covering material removed from the fire exclusion zone to restore
  compliance.
. The inspectors identified a Green noncited violation of Facility Operating  
  The licensee documented this violation in Condition Report CR-GGN-2011-00455. Its
License Condition 2.C(41), involving the failure to ensure that transient combustible were  
  short-term corrective actions included removing the combustible material from the area.
not stored in the fire exclusion zone near the independent spent fuel storage installation.  
                                          -9-                                  Enclosure
Description
. On January 24, 2011, the inspectors performed a quarterly fire protection  
inspection of independent spent fuel storage installation. The inspectors identified a  
large air conditioner with combustible material covering it located in the fire exclusion  
zone that appeared to be within 60 feet of the dry fuel storage pad. The inspectors  
brought this to the attention of the work center senior reactor operator. The work center  
senior reactor operator contacted the site fire engineer, who walked down the fire  
exclusion zone and determined that the combustible material covering the air conditioner  
was within the 60 feet of the dry fuel storage pad, which is in violation of plant procedural  
requirements. The inspectors determined through interviews that the material had been  
placed there the day before by the maintenance department. The site had the air  
conditioner and the covering material removed from the fire exclusion zone to restore  
compliance.  
The licensee documented this violation in Condition Report CR-GGN-2011-00455. Its  
short-term corrective actions included removing the combustible material from the area.  


    Analysis. The inspectors determined that the failure to follow fire protection procedures
    developed for control of transient combustible material stored near the dry spent fuel
    storage pad was a performance deficiency. This finding was more than minor because it
- 10 -
    was associated human performance attribute of the Barrier Integrity Cornerstone to
Enclosure
    provide reasonable assurance that physical design barriers protect the public from
Analysis. The inspectors determined that the failure to follow fire protection procedures  
    radionuclide releases caused by accidents or events. Using Manual Chapter 0609,
developed for control of transient combustible material stored near the dry spent fuel  
    Appendix F, Fire Protection Significance Determination Process, the inspectors
storage pad was a performance deficiency. This finding was more than minor because it  
    determined that the finding impacted the fire prevention and administrative controls
was associated human performance attribute of the Barrier Integrity Cornerstone to  
    category. The inspectors assigned a low degradation rating due to the fact that the
provide reasonable assurance that physical design barriers protect the public from  
    amount of combustible material in the area was minimal. The inspectors concluded that
radionuclide releases caused by accidents or events. Using Manual Chapter 0609,  
    the finding was of very low safety significance (Green) due to the fact there were no fire
Appendix F, Fire Protection Significance Determination Process, the inspectors  
    ignition sources in the area. The finding has a crosscutting aspect in the area of human
determined that the finding impacted the fire prevention and administrative controls  
    performance associated with the work practices component because the licensee failed
category. The inspectors assigned a low degradation rating due to the fact that the  
    to effectively communicate expectations regarding storage of combustible material near
amount of combustible material in the area was minimal. The inspectors concluded that  
    the dry fuel storage pad. [H.4(b)]
the finding was of very low safety significance (Green) due to the fact there were no fire  
    Enforcement. Grand Gulf Nuclear Station Facility Operating License Condition 2.C(41)
ignition sources in the area. The finding has a crosscutting aspect in the area of human  
    states, in part, that the plant shall implement and maintain in effect all provisions of the
performance associated with the work practices component because the licensee failed  
    Fire Protection Program as described in the UFSAR. UFSAR Section 9B,
to effectively communicate expectations regarding storage of combustible material near  
    Administrative Controls, section 9B.6.a, governs the handling and limits the use of
the dry fuel storage pad. [H.4(b)]  
    ordinary combustible materials in safety related areas. Fire area 59, defined as the yard,
    contains the fire exclusion area next to the dry fuel storage pad and prohibits the storage
Enforcement. Grand Gulf Nuclear Station Facility Operating License Condition 2.C(41)  
    of any combustible material in this area. Contrary to this, on January 23, 2011, the
states, in part, that the plant shall implement and maintain in effect all provisions of the  
    licensee stored combustible material inside the transient combustible exclusion zone
Fire Protection Program as described in the UFSAR. UFSAR Section 9B,  
    near the dry fuel storage pad. The licensee restored compliance by removing the
Administrative Controls, section 9B.6.a, governs the handling and limits the use of  
    material from the area on January 25, 2011. Because the finding was of very low safety
ordinary combustible materials in safety related areas. Fire area 59, defined as the yard,  
    significance (Green) and was documented in the licensees corrective action program as
contains the fire exclusion area next to the dry fuel storage pad and prohibits the storage  
    CR-GGN-2011-0455, this finding is being treated as a noncited violation (NCV)
of any combustible material in this area. Contrary to this, on January 23, 2011, the  
    consistent with Section VI.A of the NRC Enforcement Policy:
licensee stored combustible material inside the transient combustible exclusion zone  
    NCV 05000416/2011002-01; Transient Combustible Stored in the Fire Exclusion Zone
near the dry fuel storage pad. The licensee restored compliance by removing the  
    Near the Independent Spent Fuel Storage Installation.
material from the area on January 25, 2011. Because the finding was of very low safety  
1R06 Flood Protection Measures (71111.06)
significance (Green) and was documented in the licensees corrective action program as  
  a. Inspection Scope
CR-GGN-2011-0455, this finding is being treated as a noncited violation (NCV)  
    The inspectors reviewed the flooding analysis, and plant procedures to assess seasonal
consistent with Section VI.A of the NRC Enforcement Policy:
    susceptibilities involving internal flooding; reviewed the Updated Final Safety Analysis
NCV 05000416/2011002-01; Transient Combustible Stored in the Fire Exclusion Zone  
    Report and corrective action program to determine if licensee personnel identified and
Near the Independent Spent Fuel Storage Installation.  
    corrected flooding problems; inspected underground bunkers/manholes to verify the
    adequacy of sump pumps, level alarm circuits, cable splices subject to submergence,
1R06 Flood Protection Measures (71111.06)  
    and drainage for bunkers/manholes; subject to flooding that contain cables whose failure
a.  
    could disable risk-significant equipment. The inspectors walked down the areas listed
The inspectors reviewed the flooding analysis, and plant procedures to assess seasonal  
    below. Specific documents reviewed during this inspection are listed in the attachment.
susceptibilities involving internal flooding; reviewed the Updated Final Safety Analysis  
    *       January 11, 2011, division 1 and 2 standby service water manholes
Report and corrective action program to determine if licensee personnel identified and  
                                            - 10 -                                Enclosure
corrected flooding problems; inspected underground bunkers/manholes to verify the  
adequacy of sump pumps, level alarm circuits, cable splices subject to submergence,  
and drainage for bunkers/manholes; subject to flooding that contain cables whose failure  
could disable risk-significant equipment. The inspectors walked down the areas listed  
below. Specific documents reviewed during this inspection are listed in the attachment.  
Inspection Scope
*  
January 11, 2011, division 1 and 2 standby service water manholes  


    These activities constitute completion of one bunker/manhole sample as defined in
    Inspection Procedure 71111.06-05.
  b. Findings
- 11 -
    No findings were identified.
Enclosure
1R07 Heat Sink Performance (71111.07)
These activities constitute completion of one bunker/manhole sample as defined in  
  a. Inspection Scope
Inspection Procedure 71111.06-05.  
    The inspectors reviewed licensee programs, verified performance against industry
    standards, and reviewed critical operating parameters and maintenance records for the
b.  
    Division 1 emergency diesel generator jacket water and lube oil heat exchangers. The
No findings were identified.  
    inspectors verified that performance tests were satisfactorily conducted for heat
Findings
    exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the
    periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger
1R07 Heat Sink Performance (71111.07)  
    Performance Monitoring Guidelines; the licensee properly utilized biofouling controls;
a.  
    the licensees heat exchanger inspections adequately assessed the state of cleanliness
The inspectors reviewed licensee programs, verified performance against industry  
    of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65,
standards, and reviewed critical operating parameters and maintenance records for the  
    Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power
Division 1 emergency diesel generator jacket water and lube oil heat exchangers. The  
    Plants. Specific documents reviewed during this inspection are listed in the attachment.
inspectors verified that performance tests were satisfactorily conducted for heat  
    These activities constitute completion of one heat sink inspection sample as defined in
exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the  
    Inspection Procedure 71111.07-05.
periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger  
  b. Findings
Performance Monitoring Guidelines; the licensee properly utilized biofouling controls;  
    No findings were identified.
the licensees heat exchanger inspections adequately assessed the state of cleanliness  
1R11 Licensed Operator Requalification Program (71111.11)
of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65,  
  a. Inspection Scope
Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power  
    On January 31, 2011, the inspectors observed a crew of licensed operators in the plants
Plants. Specific documents reviewed during this inspection are listed in the attachment.  
    simulator to verify that operator performance was adequate, evaluators were identifying
Inspection Scope
    and documenting crew performance problems and training was being conducted in
    accordance with licensee procedures. The inspectors evaluated the following areas:
These activities constitute completion of one heat sink inspection sample as defined in  
    *       Licensed operator performance
Inspection Procedure 71111.07-05.  
    *       Crews clarity and formality of communications
    *       Crews ability to take timely actions in the conservative direction
b.  
    *       Crews prioritization, interpretation, and verification of annunciator alarms
    *       Crews correct use and implementation of abnormal and emergency procedures
Findings  
                                          - 11 -                                Enclosure
No findings were identified.  
1R11 Licensed Operator Requalification Program (71111.11)  
a.  
On January 31, 2011, the inspectors observed a crew of licensed operators in the plants  
simulator to verify that operator performance was adequate, evaluators were identifying  
and documenting crew performance problems and training was being conducted in  
accordance with licensee procedures. The inspectors evaluated the following areas:
Inspection Scope
*  
Licensed operator performance  
*  
Crews clarity and formality of communications  
*  
Crews ability to take timely actions in the conservative direction  
*  
Crews prioritization, interpretation, and verification of annunciator alarms  
*  
Crews correct use and implementation of abnormal and emergency procedures  


    *       Control board manipulations
    *       Oversight and direction from supervisors
    *       Crews ability to identify and implement appropriate technical specification
- 12 -
            actions and emergency plan actions and notifications
Enclosure
    The inspectors compared the crews performance in these areas to preestablished
    operator action expectations and successful critical task completion requirements.
*  
    Specific documents reviewed during this inspection are listed in the attachment.
Control board manipulations  
    These activities constitute completion of one quarterly licensed-operator requalification
    program sample as defined in Inspection Procedure 71111.11.
*  
  b. Findings
Oversight and direction from supervisors  
    No findings were identified.
1R12 Maintenance Effectiveness (71111.12)
*  
  a. Inspection Scope
Crews ability to identify and implement appropriate technical specification  
    The inspectors evaluated degraded performance issues involving the following risk
actions and emergency plan actions and notifications  
    significant systems:
    *       Appendix R emergency lighting units (Z92)
The inspectors compared the crews performance in these areas to preestablished  
    *       Control room air conditioning (Z51)
operator action expectations and successful critical task completion requirements.
    *       Residual heat removal (E12)
Specific documents reviewed during this inspection are listed in the attachment.  
    The inspectors reviewed events such as where ineffective equipment maintenance has
    resulted in valid or invalid automatic actuations of engineered safeguards systems and
These activities constitute completion of one quarterly licensed-operator requalification  
    independently verified the licensee's actions to address system performance or condition
program sample as defined in Inspection Procedure 71111.11.  
    problems in terms of the following:
    *       Implementing appropriate work practices
b.  
    *       Identifying and addressing common cause failures
No findings were identified.  
    *       Scoping of systems in accordance with 10 CFR 50.65(b)
Findings
    *       Characterizing system reliability issues for performance
    *       Charging unavailability for performance
1R12 Maintenance Effectiveness (71111.12)  
    *       Trending key parameters for condition monitoring
a.  
                                          - 12 -                              Enclosure
The inspectors evaluated degraded performance issues involving the following risk  
significant systems:  
Inspection Scope
*  
Appendix R emergency lighting units (Z92)  
*  
Control room air conditioning (Z51)  
*  
Residual heat removal (E12)  
The inspectors reviewed events such as where ineffective equipment maintenance has  
resulted in valid or invalid automatic actuations of engineered safeguards systems and  
independently verified the licensee's actions to address system performance or condition  
problems in terms of the following:  
*  
Implementing appropriate work practices  
*  
Identifying and addressing common cause failures  
*  
Scoping of systems in accordance with 10 CFR 50.65(b)
*  
Characterizing system reliability issues for performance  
*  
Charging unavailability for performance  
*  
Trending key parameters for condition monitoring  


    *       Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)
    *       Verifying appropriate performance criteria for structures, systems, and
            components classified as having an adequate demonstration of performance
- 13 -
            through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as
Enclosure
            requiring the establishment of appropriate and adequate goals and corrective
*  
            actions for systems classified as not having adequate performance, as described
Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)  
            in 10 CFR 50.65(a)(1)
    The inspectors assessed performance issues with respect to the reliability, availability,
*  
    and condition monitoring of the system. In addition, the inspectors verified maintenance
Verifying appropriate performance criteria for structures, systems, and  
    effectiveness issues were entered into the corrective action program with the appropriate
components classified as having an adequate demonstration of performance  
    significance characterization. Specific documents reviewed during this inspection are
through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as  
    listed in the attachment.
requiring the establishment of appropriate and adequate goals and corrective  
    These activities constitute completion of three quarterly maintenance effectiveness
actions for systems classified as not having adequate performance, as described  
    samples as defined in Inspection Procedure 71111.12-05.
in 10 CFR 50.65(a)(1)  
b. Findings
.1 Failure to Update Available Low Pressure Cooling Injection Loops in the Updated Final
The inspectors assessed performance issues with respect to the reliability, availability,  
    Safety Analysis Report
and condition monitoring of the system. In addition, the inspectors verified maintenance  
    Introduction. Inspectors identified a Severity Level IV, noncited violation for the
effectiveness issues were entered into the corrective action program with the appropriate  
    licensees failure to update the final (updated) safety analysis report in accordance with
significance characterization. Specific documents reviewed during this inspection are  
    10 CFR 50.71(e)(4). Specifically, the licensee failed to update Section 6.3, Emergency
listed in the attachment.  
    Core Cooling Systems, to appropriately reflect the available emergency core cooling
    equipment during shutdown cooling operations in Mode 3.
These activities constitute completion of three quarterly maintenance effectiveness  
    Description. On February 28, 2011, while reviewing the updated final safety analysis
samples as defined in Inspection Procedure 71111.12-05.  
    report for a maintenance effectiveness inspection of the residual heat removal system,
    the inspectors determined that Section 6.3.1.1.1.e, Emergency Core Cooling Systems,
b.  
    states, The ECCS is designed to satisfy all criteria specified in Section 6.3 for any
.1 Failure to Update Available Low Pressure Cooling Injection Loops in the Updated Final  
    normal mode of reactor operation. Additionally, Section 6.3.1.1.2.d states, In the event
Safety Analysis Report  
    of a break in a pipe that is part of the reactor coolant pressure boundary, no single active
Findings
    component failure in the emergency core cooling system shall prevent automatic
Introduction. Inspectors identified a Severity Level IV, noncited violation for the  
    initiation and successful operation of less than the following combination of emergency
licensees failure to update the final (updated) safety analysis report in accordance with  
    core cooling system equipment: 1) Three low pressure coolant injection loops, the low
10 CFR 50.71(e)(4). Specifically, the licensee failed to update Section 6.3, Emergency  
    pressure core spray and the automatic depressurization system (i.e., high pressure core
Core Cooling Systems, to appropriately reflect the available emergency core cooling  
    spray failure); 2) Two low pressure coolant injection loops, the high pressure core spray
equipment during shutdown cooling operations in Mode 3.  
    and the automatic depressurization system (i.e., low pressure core spray diesel
Description. On February 28, 2011, while reviewing the updated final safety analysis  
    generator failure); and 3) One low pressure coolant injection loop, the low pressure core
report for a maintenance effectiveness inspection of the residual heat removal system,  
    spray, the high pressure core spray and automatic depressurization system (i.e., low
the inspectors determined that Section 6.3.1.1.1.e, Emergency Core Cooling Systems,  
    pressure coolant injection diesel generator failure).
states, The ECCS is designed to satisfy all criteria specified in Section 6.3 for any  
    Procedure 03-1-01-3, Plant Shutdown, Revision 118, Section 6.14 states, When
normal mode of reactor operation. Additionally, Section 6.3.1.1.2.d states, In the event  
    shutdown cooling is placed in service at less than 135 psig, then the associated
of a break in a pipe that is part of the reactor coolant pressure boundary, no single active  
    containment spray and low pressure coolant injection systems may be considered
component failure in the emergency core cooling system shall prevent automatic  
                                          - 13 -                                Enclosure
initiation and successful operation of less than the following combination of emergency  
core cooling system equipment: 1) Three low pressure coolant injection loops, the low  
pressure core spray and the automatic depressurization system (i.e., high pressure core  
spray failure); 2) Two low pressure coolant injection loops, the high pressure core spray  
and the automatic depressurization system (i.e., low pressure core spray diesel  
generator failure); and 3) One low pressure coolant injection loop, the low pressure core  
spray, the high pressure core spray and automatic depressurization system (i.e., low  
pressure coolant injection diesel generator failure).  
Procedure 03-1-01-3, Plant Shutdown, Revision 118, Section 6.14 states, When  
shutdown cooling is placed in service at less than 135 psig, then the associated  
containment spray and low pressure coolant injection systems may be considered  


  operable if capable of being manually realigned and not otherwise inoperable.
  Inspectors noted that because the residual heat removal system that provides shutdown
  cooling in Mode 3 is not available for automatic initiation (must be manually realigned) of
- 14 -
  low pressure coolant injection, in the event of a reactor coolant system pipe break, that
Enclosure
  the aforementioned statements in Section 6.3 did not appropriately reflect the available
operable if capable of being manually realigned and not otherwise inoperable.
  emergency core cooling equipment during shutdown cooling operations. In other words,
Inspectors noted that because the residual heat removal system that provides shutdown  
  the combinations of emergency core cooling equipment available for automatic initiation
cooling in Mode 3 is not available for automatic initiation (must be manually realigned) of  
  would include one less low pressure coolant injection loop.
low pressure coolant injection, in the event of a reactor coolant system pipe break, that  
  The licensee entered this issue into their corrective actions program as Condition Report
the aforementioned statements in Section 6.3 did not appropriately reflect the available  
  CR-GGN-2011-01631. The licensee planned to take actions to update the updated final
emergency core cooling equipment during shutdown cooling operations. In other words,  
  safety analysis report at the next scheduled revision.
the combinations of emergency core cooling equipment available for automatic initiation  
  Analysis. The failure of licensing personnel to update the final safety analysis report to
would include one less low pressure coolant injection loop.  
  reflect the available low pressure coolant injection loops for automatic initiation during
The licensee entered this issue into their corrective actions program as Condition Report  
  shutdown cooling operations in Mode 3 was a performance deficiency. This finding was
CR-GGN-2011-01631. The licensee planned to take actions to update the updated final  
  evaluated using traditional enforcement because it had the potential for impacting the
safety analysis report at the next scheduled revision.  
  NRCs ability to perform its regulatory function. The inspectors used the NRC
Analysis. The failure of licensing personnel to update the final safety analysis report to  
  Enforcement Policy, dated September 30, 2010, to evaluate the significance of this
reflect the available low pressure coolant injection loops for automatic initiation during  
  violation. Consistent with the NRC Enforcement Policy, this finding was determined to
shutdown cooling operations in Mode 3 was a performance deficiency. This finding was  
  be a Severity Level IV noncited violation. This finding had no crosscutting aspect as it
evaluated using traditional enforcement because it had the potential for impacting the  
  was associated with a traditional enforcement violation.
NRCs ability to perform its regulatory function. The inspectors used the NRC  
  Enforcement. Title 10 CFR 50.71(e)(4) requires the final safety analysis report be
Enforcement Policy, dated September 30, 2010, to evaluate the significance of this  
  updated, at intervals not exceeding 24 months, and states in part, the revisions must
violation. Consistent with the NRC Enforcement Policy, this finding was determined to  
  reflect all changes made in the facility or procedures described in the FSAR. Contrary
be a Severity Level IV noncited violation. This finding had no crosscutting aspect as it  
  to the above, licensing personnel failed to update the original revision of the final safety
was associated with a traditional enforcement violation.  
  analysis report to reflect the actual number of low pressure coolant injection loops
Enforcement. Title 10 CFR 50.71(e)(4) requires the final safety analysis report be  
  available for automatic initiation during shutdown cooling operations in Mode 3.
updated, at intervals not exceeding 24 months, and states in part, the revisions must  
  Because the finding is of very low safety significance and has been entered into the
reflect all changes made in the facility or procedures described in the FSAR. Contrary  
  corrective action program as Condition Report CR-GGN-2011-01631, this violation is
to the above, licensing personnel failed to update the original revision of the final safety  
  being treated as a noncited violation consistent with the NRC Enforcement Policy:
analysis report to reflect the actual number of low pressure coolant injection loops  
  NCV 0500416/20011002-02, "Failure to Update Available Low Pressure Coolant
available for automatic initiation during shutdown cooling operations in Mode 3.
  Injection Loops in the Updated Final Safety Analysis Report."
Because the finding is of very low safety significance and has been entered into the  
.2 Failure to Demonstrate Maintenance Effectiveness of Train B Control Room Air
corrective action program as Condition Report CR-GGN-2011-01631, this violation is  
  Conditioner
being treated as a noncited violation consistent with the NRC Enforcement Policy:  
  Introduction. The inspectors identified a Green noncited violation of 10 CFR Part
NCV 0500416/20011002-02, "Failure to Update Available Low Pressure Coolant  
  50.65(a)(2) for the failure to demonstrate that the performance of the train B control
Injection Loops in the Updated Final Safety Analysis Report."  
  room air conditioner was being effectively controlled through the performance of
  appropriate preventive maintenance.
.2 Failure to Demonstrate Maintenance Effectiveness of Train B Control Room Air  
  Description. On March 2, 2011, the inspectors performed a maintenance effectiveness
Conditioner  
  inspection of the control room air conditioning system. Inspectors determined that on
Introduction. The inspectors identified a Green noncited violation of 10 CFR Part  
  February 3, 2010, the train B control room air conditioner compressor was replaced with
50.65(a)(2) for the failure to demonstrate that the performance of the train B control  
  a remanufactured compressor as part of annual preventative maintenance of the
room air conditioner was being effectively controlled through the performance of  
  system. On March 27, 2010, the control room air conditioner compressor tripped on low
appropriate preventive maintenance.  
                                        - 14 -                                Enclosure
Description. On March 2, 2011, the inspectors performed a maintenance effectiveness  
inspection of the control room air conditioning system. Inspectors determined that on  
February 3, 2010, the train B control room air conditioner compressor was replaced with  
a remanufactured compressor as part of annual preventative maintenance of the  
system. On March 27, 2010, the control room air conditioner compressor tripped on low  


usable oil pressure. The licensees investigation revealed that the compressor pencil
strainer was approximately fifty percent covered with unidentified contaminants. Similar
contaminants were identified on the oil sump strainer. The licensee concluded that the
- 15 -
compressor had been installed with contaminants inside the lower half of the
Enclosure
compressor, and subsequently replaced the remanufactured compressor on April 1,
usable oil pressure. The licensees investigation revealed that the compressor pencil  
2010, with a newly rebuilt compressor. System engineering did not classify this event as
strainer was approximately fifty percent covered with unidentified contaminants. Similar  
a maintenance rule functional failure even though operations had declared the train
contaminants were identified on the oil sump strainer. The licensee concluded that the  
inoperable and also stated in their operability determination that it could not meet its 30
compressor had been installed with contaminants inside the lower half of the  
day mission time.
compressor, and subsequently replaced the remanufactured compressor on April 1,  
The train B control room air conditioner compressor subsequently either tripped or failed
2010, with a newly rebuilt compressor. System engineering did not classify this event as  
to properly cool the control room, due to low usable oil pressure, on three separate
a maintenance rule functional failure even though operations had declared the train  
occasions (once in April, once May, and once in June). In response to the June failure,
inoperable and also stated in their operability determination that it could not meet its 30  
the licensee performed extensive maintenance on the train B control room air
day mission time.  
conditioner compressor, which included installing a five micron suction line filter in the
The train B control room air conditioner compressor subsequently either tripped or failed  
system. Additionally, all three events were identified as maintenance rule functional
to properly cool the control room, due to low usable oil pressure, on three separate  
failures attributed to foreign material fouling in the system, which would have resulted in
occasions (once in April, once May, and once in June). In response to the June failure,  
the performance criteria being exceeded (less than or equal to two maintenance rule
the licensee performed extensive maintenance on the train B control room air  
functional failure events or as a repeat functional failure). However, the sites
conditioner compressor, which included installing a five micron suction line filter in the  
maintenance rule coordinator informed the inspectors that the first two events in April
system. Additionally, all three events were identified as maintenance rule functional  
and May were not counted toward the criteria because they were from the same cause
failures attributed to foreign material fouling in the system, which would have resulted in  
as the June event and; therefore, they would all be counted as one failure even thought
the performance criteria being exceeded (less than or equal to two maintenance rule  
the train was returned to service each time after corrective maintenance was performed
functional failure events or as a repeat functional failure). However, the sites  
and declared operable by operations. Additionally, on June 22, 2010, the train was
maintenance rule coordinator informed the inspectors that the first two events in April  
declared inoperable due to multiple Freon leaks and was classified as another
and May were not counted toward the criteria because they were from the same cause  
maintenance rule functional failure for the train. On August 10, 2010, the licensee
as the June event and; therefore, they would all be counted as one failure even thought  
performed a Maintenance Rule (a)(1) evaluation for the subject system and, based on
the train was returned to service each time after corrective maintenance was performed  
the presentation to the expert panel by system engineering, the panel only considered
and declared operable by operations. Additionally, on June 22, 2010, the train was  
two events as maintenance rule functional failures. System engineering did not count
declared inoperable due to multiple Freon leaks and was classified as another  
the one failure in March or consider the two failures in April or May. The expert panel
maintenance rule functional failure for the train. On August 10, 2010, the licensee  
only considered the failures in June due to low oil pressure and Freon leaks. Therefore
performed a Maintenance Rule (a)(1) evaluation for the subject system and, based on  
the expert panel concluded that, although the train B control room air conditioner system
the presentation to the expert panel by system engineering, the panel only considered  
had exceeded its established performance criteria for functional failure events, a number
two events as maintenance rule functional failures. System engineering did not count  
of effective corrective actions had been identified and implemented and additional
the one failure in March or consider the two failures in April or May. The expert panel  
corrective actions were not necessary; therefore, the subject system was allowed to
only considered the failures in June due to low oil pressure and Freon leaks. Therefore  
retain its (a)(2) status.
the expert panel concluded that, although the train B control room air conditioner system  
The train B control room air conditioner compressor subsequently either tripped or failed
had exceeded its established performance criteria for functional failure events, a number  
to properly cool the control room, due to low usable oil pressure, on two separate
of effective corrective actions had been identified and implemented and additional  
occasions (once in September and once in October). The October trip of the subject
corrective actions were not necessary; therefore, the subject system was allowed to  
system compressor occurred while the train A control room air conditioner was out of
retain its (a)(2) status.  
service for routine maintenance. The compressor pencil strainer and sump strainer were
The train B control room air conditioner compressor subsequently either tripped or failed  
again identified with contaminants on them. The licensee was required to make an
to properly cool the control room, due to low usable oil pressure, on two separate  
eight-hour report to the NRC and submit a licensee event report due to both trains of
occasions (once in September and once in October). The October trip of the subject  
control room air conditioner being inoperable. The licensees root cause analysis failed
system compressor occurred while the train A control room air conditioner was out of  
to identify that the train B control room air conditioner performance had not been
service for routine maintenance. The compressor pencil strainer and sump strainer were  
demonstrated through the performance of appropriate preventative maintenance; nor did
again identified with contaminants on them. The licensee was required to make an  
the root cause identify that the licensee failed to set goals and monitor the system as
eight-hour report to the NRC and submit a licensee event report due to both trains of  
                                      - 15 -                              Enclosure
control room air conditioner being inoperable. The licensees root cause analysis failed  
to identify that the train B control room air conditioner performance had not been  
demonstrated through the performance of appropriate preventative maintenance; nor did  
the root cause identify that the licensee failed to set goals and monitor the system as  


required by 10 CFR 50.65(a)(1). The train B control room air conditioner was ultimately
moved into (a)(1) status on February 4, 2011, after the subject compressor again tripped
due to low oil pressure on December 13, 2010. After this trip and upon further
- 16 -
evaluation, the licensee performed an additional corrective action that installed an in line
Enclosure
suction filter with smaller filtering diameter and larger surface area to remove foreign
required by 10 CFR 50.65(a)(1). The train B control room air conditioner was ultimately  
material from the system. They also modified the operator rounds to obtain daily
moved into (a)(1) status on February 4, 2011, after the subject compressor again tripped  
readings of differential pressure across this new filter and through calculation,
due to low oil pressure on December 13, 2010. After this trip and upon further  
determined a differential pressure necessary for the filter to be changed out and the unit
evaluation, the licensee performed an additional corrective action that installed an in line  
to be inspected for foreign materials.
suction filter with smaller filtering diameter and larger surface area to remove foreign  
The licensee entered this issue into their corrective actions program as Condition Report
material from the system. They also modified the operator rounds to obtain daily  
CR-GGN-2011-01623. From installation of the new inline suction filter to the conclusion
readings of differential pressure across this new filter and through calculation,  
of the inspection period, no additional trips of train B control room air conditioning have
determined a differential pressure necessary for the filter to be changed out and the unit  
occurred.
to be inspected for foreign materials.  
Analysis. The inspectors determined that the failure to demonstrate that the
The licensee entered this issue into their corrective actions program as Condition Report  
performance of the train B control room air conditioner was being effectively controlled
CR-GGN-2011-01623. From installation of the new inline suction filter to the conclusion  
through the performance of appropriate preventive maintenance was a performance
of the inspection period, no additional trips of train B control room air conditioning have  
deficiency. The finding was more than minor because it was associated with the
occurred.  
equipment performance attribute of the Mitigating Systems Cornerstone and adversely
Analysis. The inspectors determined that the failure to demonstrate that the  
affected the cornerstone objective to ensure the availability, reliability, and capability of
performance of the train B control room air conditioner was being effectively controlled  
systems that respond to initiating events to prevent undesirable consequences.
through the performance of appropriate preventive maintenance was a performance  
Inspectors performed a Phase 1 screening, in accordance with Inspection Manual
deficiency. The finding was more than minor because it was associated with the  
Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of
equipment performance attribute of the Mitigating Systems Cornerstone and adversely  
Findings, and determined that the finding was of very low safety significance (Green)
affected the cornerstone objective to ensure the availability, reliability, and capability of  
because it did not result in a loss of system safety function since the train A control room
systems that respond to initiating events to prevent undesirable consequences.
air conditioner remained operable. This finding had a crosscutting aspect in the area of
Inspectors performed a Phase 1 screening, in accordance with Inspection Manual  
human performance associated with the decision making component because licensee
Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of  
personnel failed to make appropriate safety-significant or risk-significant decisions to
Findings, and determined that the finding was of very low safety significance (Green)  
address the multiple failures of the train B CRAC compressor. [H.1(a)]
because it did not result in a loss of system safety function since the train A control room  
Enforcement. Title 10 CFR 50.65(a)(2), states, in part, that monitoring as specified in
air conditioner remained operable. This finding had a crosscutting aspect in the area of  
paragraph (a)(1) of this section is not required where it has been demonstrated that the
human performance associated with the decision making component because licensee  
performance or condition of a structure, system, or component is being effectively
personnel failed to make appropriate safety-significant or risk-significant decisions to  
controlled through the performance of appropriate preventative maintenance, such that
address the multiple failures of the train B CRAC compressor. [H.1(a)]  
the structure, system, or component remains capable of performing its intended
Enforcement. Title 10 CFR 50.65(a)(2), states, in part, that monitoring as specified in  
function. Contrary to the above, from March 2010 to February 2011, the licensee failed
paragraph (a)(1) of this section is not required where it has been demonstrated that the  
to demonstrate that the performance of the train B control room air conditioning system
performance or condition of a structure, system, or component is being effectively  
was effectively controlled through the performance of appropriate preventative
controlled through the performance of appropriate preventative maintenance, such that  
maintenance. This finding was entered into the licensees corrective action program as
the structure, system, or component remains capable of performing its intended  
Condition Report CR-GGN-2011-01623. Because this finding was determined to be of
function. Contrary to the above, from March 2010 to February 2011, the licensee failed  
very low safety significance and was entered into the licensees corrective action
to demonstrate that the performance of the train B control room air conditioning system  
program, this violation is being treated as a noncited violation consistent with the NRC
was effectively controlled through the performance of appropriate preventative  
Enforcement Policy: NCV 05000285/2011002-03, Failure to Demonstrate Maintenance
maintenance. This finding was entered into the licensees corrective action program as  
Effectiveness of Train B Control Room Air Conditioner.
Condition Report CR-GGN-2011-01623. Because this finding was determined to be of  
                                      - 16 -                                Enclosure
very low safety significance and was entered into the licensees corrective action  
program, this violation is being treated as a noncited violation consistent with the NRC  
Enforcement Policy: NCV 05000285/2011002-03, Failure to Demonstrate Maintenance  
Effectiveness of Train B Control Room Air Conditioner.  


1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
  a. Inspection Scope
    The inspectors reviewed licensee personnel's evaluation and management of plant risk
- 17 -
    for the maintenance and emergent work activities affecting risk-significant and safety-
Enclosure
    related equipment listed below to verify that the appropriate risk assessments were
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
    performed prior to removing equipment for work:
a.  
    *       On January 9, 2011, during an ice storm requiring the plant to enter a yellow risk
The inspectors reviewed licensee personnel's evaluation and management of plant risk  
              condition and enter their off normal event procedure for severe weather.
for the maintenance and emergent work activities affecting risk-significant and safety-
    *       On February 3, 2011, during an ice storm requiring the plant to enter a yellow risk
related equipment listed below to verify that the appropriate risk assessments were  
              condition and enter their off normal event procedure for severe weather. The
performed prior to removing equipment for work:  
              weather required the site to cancel work and monitor their safety related standby
Inspection Scope
              service water system for icing conditions.
    *       On February 9, 2011, during a winter storm, while a divisions 1 diesel generator
*  
              and residual heat removal A were out for planned maintenance outage requiring
On January 9, 2011, during an ice storm requiring the plant to enter a yellow risk  
              the plant to enter orange risk.
condition and enter their off normal event procedure for severe weather.  
    *       On February 28, 2011, during the accidental unearthing of energized plant
              service water pump cables, no consequence to the plant but resulted in work
*  
              stoppage and evaluation of risk status for the site.
On February 3, 2011, during an ice storm requiring the plant to enter a yellow risk  
    *       On March 8-9, 2011, with an emergent issue with the division 1 diesel generator
condition and enter their off normal event procedure for severe weather. The  
              and a tornado watch issued for the area requiring the plant to enter yellow risk.
weather required the site to cancel work and monitor their safety related standby  
              The site entered their severe weather off normal procedure; this procedure
service water system for icing conditions.  
              required the site to secure from half scram surveillances.
    The inspectors selected these activities based on potential risk significance relative to
*  
    the reactor safety cornerstones. As applicable for each activity, the inspectors verified
On February 9, 2011, during a winter storm, while a divisions 1 diesel generator  
    that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)
and residual heat removal A were out for planned maintenance outage requiring  
    and that the assessments were accurate and complete. When licensee personnel
the plant to enter orange risk.  
    performed emergent work, the inspectors verified that the licensee personnel promptly
    assessed and managed plant risk. The inspectors reviewed the scope of maintenance
*  
    work, discussed the results of the assessment with the licensee's probabilistic risk
On February 28, 2011, during the accidental unearthing of energized plant  
    analyst or shift technical advisor, and verified plant conditions were consistent with the
service water pump cables, no consequence to the plant but resulted in work  
    risk assessment. The inspectors also reviewed the technical specification requirements
stoppage and evaluation of risk status for the site.  
    and inspected portions of redundant safety systems, when applicable, to verify risk
    analysis assumptions were valid and applicable requirements were met. Specific
*  
    documents reviewed during this inspection are listed in the attachment.
On March 8-9, 2011, with an emergent issue with the division 1 diesel generator  
    These activities constitute completion of five emergent work control inspection samples
and a tornado watch issued for the area requiring the plant to enter yellow risk.
    as defined in Inspection Procedure 71111.13-05.
The site entered their severe weather off normal procedure; this procedure  
                                          - 17 -                              Enclosure
required the site to secure from half scram surveillances.  
The inspectors selected these activities based on potential risk significance relative to  
the reactor safety cornerstones. As applicable for each activity, the inspectors verified  
that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)  
and that the assessments were accurate and complete. When licensee personnel  
performed emergent work, the inspectors verified that the licensee personnel promptly  
assessed and managed plant risk. The inspectors reviewed the scope of maintenance  
work, discussed the results of the assessment with the licensee's probabilistic risk  
analyst or shift technical advisor, and verified plant conditions were consistent with the  
risk assessment. The inspectors also reviewed the technical specification requirements  
and inspected portions of redundant safety systems, when applicable, to verify risk  
analysis assumptions were valid and applicable requirements were met. Specific  
documents reviewed during this inspection are listed in the attachment.  
These activities constitute completion of five emergent work control inspection samples  
as defined in Inspection Procedure 71111.13-05.  


  b. Findings
    No findings were identified.
1R15 Operability Evaluations (71111.15)
- 18 -
  a. Inspection Scope
Enclosure
    The inspectors reviewed the following issues:
b.  
    *       Division 3 high pressure core spray diesel generator outside air fan temperature
No findings were identified.  
            switch fluctuating
Findings
    *       Train A standby service water drift eliminator support base plate corrosion and
            missing brass bolts
1R15 Operability Evaluations (71111.15)  
    *       Train A standby service water valve P41-F299A flange degradation
a.  
    *       Residual heat removal equipment area temperature high/inoperable due to
The inspectors reviewed the following issues:  
            temperature switch
Inspection Scope
    *       Site fire truck inoperable
    *       Division 1 diesel generator auxiliary oil pump not obtaining procedural pressures
*  
            during pre-lube prior to surveillance run
Division 3 high pressure core spray diesel generator outside air fan temperature  
    The inspectors selected these potential operability issues based on the risk significance
switch fluctuating  
    of the associated components and systems. The inspectors evaluated the technical
    adequacy of the evaluations to ensure that technical specification operability was
*  
    properly justified and the subject component or system remained available such that no
Train A standby service water drift eliminator support base plate corrosion and  
    unrecognized increase in risk occurred. The inspectors compared the operability and
missing brass bolts  
    design criteria in the appropriate sections of the technical specifications and UFSAR to
    the licensee personnels evaluations to determine whether the components or systems
*  
    were operable. Where compensatory measures were required to maintain operability,
Train A standby service water valve P41-F299A flange degradation  
    the inspectors determined whether the measures in place would function as intended
    and were properly controlled. The inspectors determined, where appropriate,
*  
    compliance with bounding limitations associated with the evaluations. Additionally, the
Residual heat removal equipment area temperature high/inoperable due to  
    inspectors also reviewed a sampling of corrective action documents to verify that the
temperature switch  
    licensee was identifying and correcting any deficiencies associated with operability
    evaluations. Specific documents reviewed during this inspection are listed in the
*  
    attachment.
Site fire truck inoperable
    These activities constitute completion of six operability evaluations inspection samples
    as defined in Inspection Procedure 71111.15-04
*  
                                        - 18 -                                Enclosure
Division 1 diesel generator auxiliary oil pump not obtaining procedural pressures  
during pre-lube prior to surveillance run  
The inspectors selected these potential operability issues based on the risk significance  
of the associated components and systems. The inspectors evaluated the technical  
adequacy of the evaluations to ensure that technical specification operability was  
properly justified and the subject component or system remained available such that no  
unrecognized increase in risk occurred. The inspectors compared the operability and  
design criteria in the appropriate sections of the technical specifications and UFSAR to  
the licensee personnels evaluations to determine whether the components or systems  
were operable. Where compensatory measures were required to maintain operability,  
the inspectors determined whether the measures in place would function as intended  
and were properly controlled. The inspectors determined, where appropriate,  
compliance with bounding limitations associated with the evaluations. Additionally, the  
inspectors also reviewed a sampling of corrective action documents to verify that the  
licensee was identifying and correcting any deficiencies associated with operability  
evaluations. Specific documents reviewed during this inspection are listed in the  
attachment.  
These activities constitute completion of six operability evaluations inspection samples  
as defined in Inspection Procedure 71111.15-04  


  b. Findings
    No findings were identified.
1R18 Plant Modifications (71111.18)
- 19 -
  a. Inspection Scope
Enclosure
    To verify that the safety functions of important safety systems were not degraded, the
b.  
    inspectors reviewed the following temporary modifications:
No findings were identified.  
    *       Temporary Modification for RWCU A/B Leak Detection (EC 22625 & EC 22635)
Findings
    *       Temporary Modification to install bypass signals for B first stage Pressure
            Sensor (EC22768)
1R18 Plant Modifications (71111.18)  
    The inspectors reviewed the temporary modifications and the associated safety-
a.  
    evaluation screening against the system design bases documentation, including the
To verify that the safety functions of important safety systems were not degraded, the  
    updated final safety analysis report and the technical specifications, and verified that the
inspectors reviewed the following temporary modifications:  
    modification did not adversely affect the system operability/availability. The inspectors
Inspection Scope
    also verified that the installation and restoration were consistent with the modification
    documents and that configuration control was adequate. Additionally, the inspectors
*  
    verified that the temporary modification was identified on control room drawings,
Temporary Modification for RWCU A/B Leak Detection (EC 22625 & EC 22635)  
    appropriate tags were placed on the affected equipment, and licensee personnel
    evaluated the combined effects on mitigating systems and the integrity of radiological
*  
    barriers.
Temporary Modification to install bypass signals for B first stage Pressure  
    These activities constitute completion of two samples for temporary plant modifications
Sensor (EC22768)  
    as defined in Inspection Procedure 71111.18-05.
  b. Findings
The inspectors reviewed the temporary modifications and the associated safety-
    No findings were identified.
evaluation screening against the system design bases documentation, including the  
1R19 Postmaintenance Testing (71111.19)
updated final safety analysis report and the technical specifications, and verified that the  
  a. Inspection Scope
modification did not adversely affect the system operability/availability. The inspectors  
    The inspectors reviewed the following postmaintenance activities to verify that
also verified that the installation and restoration were consistent with the modification  
    procedures and test activities were adequate to ensure system operability and functional
documents and that configuration control was adequate. Additionally, the inspectors  
    capability:
verified that the temporary modification was identified on control room drawings,  
    *       For standby liquid B after a maintenance outage
appropriate tags were placed on the affected equipment, and licensee personnel  
    *       For reactor protection motor generator B after required maintenance
evaluated the combined effects on mitigating systems and the integrity of radiological  
    *       For residual heat removal system A after a maintenance outage
barriers.  
                                          - 19 -                                Enclosure
These activities constitute completion of two samples for temporary plant modifications  
as defined in Inspection Procedure 71111.18-05.  
b.  
No findings were identified.  
Findings
1R19 Postmaintenance Testing (71111.19)  
a.  
The inspectors reviewed the following postmaintenance activities to verify that  
procedures and test activities were adequate to ensure system operability and functional  
capability:  
Inspection Scope
*  
For standby liquid B after a maintenance outage  
*  
For reactor protection motor generator B after required maintenance  
*  
For residual heat removal system A after a maintenance outage  


    *       For standby service water system A after a maintenance outage
    *       For division 1 diesel generator after a maintenance outage
    *       For high pressure core spray minimum flow valve 1E22-F012 after corrective
- 20 -
              maintenance
Enclosure
    The inspectors selected these activities based upon the structure, system, or
*  
    component's ability to affect risk. The inspectors evaluated these activities for the
For standby service water system A after a maintenance outage  
    following (as applicable):
    *       The effect of testing on the plant had been adequately addressed; testing was
*  
              adequate for the maintenance performed
For division 1 diesel generator after a maintenance outage  
    *       Acceptance criteria were clear and demonstrated operational readiness; test
              instrumentation was appropriate
*  
    The inspectors evaluated the activities against the technical specifications, the UFSAR,
For high pressure core spray minimum flow valve 1E22-F012 after corrective  
    10 CFR Part 50 requirements, licensee procedures, and various NRC generic
maintenance  
    communications to ensure that the test results adequately ensured that the equipment
    met the licensing basis and design requirements. In addition, the inspectors reviewed
The inspectors selected these activities based upon the structure, system, or  
    corrective action documents associated with postmaintenance tests to determine
component's ability to affect risk. The inspectors evaluated these activities for the  
    whether the licensee was identifying problems and entering them in the corrective action
following (as applicable):  
    program and that the problems were being corrected commensurate with their
    importance to safety. Specific documents reviewed during this inspection are listed in
*  
    the attachment.
The effect of testing on the plant had been adequately addressed; testing was  
    These activities constitute completion of six postmaintenance testing inspection samples
adequate for the maintenance performed  
    as defined in Inspection Procedure 71111.19-05.
  b. Findings
*  
    No findings were identified.
Acceptance criteria were clear and demonstrated operational readiness; test  
1R22 Surveillance Testing (71111.22)
instrumentation was appropriate  
  a. Inspection Scope
    The inspectors reviewed the UFSAR, procedure requirements, and technical
The inspectors evaluated the activities against the technical specifications, the UFSAR,  
    specifications to ensure that the surveillance activities listed below demonstrated that the
10 CFR Part 50 requirements, licensee procedures, and various NRC generic  
    systems, structures, and/or components tested were capable of performing their
communications to ensure that the test results adequately ensured that the equipment  
    intended safety functions. The inspectors either witnessed or reviewed test data to
met the licensing basis and design requirements. In addition, the inspectors reviewed  
    verify that the significant surveillance test attributes were adequate to address the
corrective action documents associated with postmaintenance tests to determine  
    following:
whether the licensee was identifying problems and entering them in the corrective action  
    *       Preconditioning
program and that the problems were being corrected commensurate with their  
                                          - 20 -                              Enclosure
importance to safety. Specific documents reviewed during this inspection are listed in  
the attachment.  
These activities constitute completion of six postmaintenance testing inspection samples  
as defined in Inspection Procedure 71111.19-05.  
b.  
No findings were identified.  
Findings
1R22 Surveillance Testing (71111.22)  
a.  
Inspection Scope  
The inspectors reviewed the UFSAR, procedure requirements, and technical  
specifications to ensure that the surveillance activities listed below demonstrated that the  
systems, structures, and/or components tested were capable of performing their  
intended safety functions. The inspectors either witnessed or reviewed test data to  
verify that the significant surveillance test attributes were adequate to address the  
following:  
*  
Preconditioning  


*       Evaluation of testing impact on the plant
*       Acceptance criteria
*       Test equipment
- 21 -
*       Procedures
Enclosure
*       Test data
*  
*       Testing frequency and method demonstrated technical specification operability
Evaluation of testing impact on the plant  
*       Test equipment removal
*       Restoration of plant systems
*  
*       Updating of performance indicator data
Acceptance criteria  
*       Engineering evaluations, root causes, and bases for returning tested systems,
        structures, and components not meeting the test acceptance criteria were correct
*  
*       Reference setting data
Test equipment  
*       Annunciators and alarms setpoints
The inspectors also verified that licensee personnel identified and implemented any
*  
needed corrective actions associated with the surveillance testing.
Procedures  
*       On January 7, 2011, reactor coolant system leakage detection surveillance
*       On February 4, 2011, inservice test of residual heat removal system B quarterly
*  
*       On February 23, 2011, reactor coolant routine chemistry surveillance
Test data  
*       On March 2, 2011, fuel handling area ventilation exhaust radiation monitor time
        response test
*  
*       On March 10, 2011, division 1 diesel generator monthly surveillance
Testing frequency and method demonstrated technical specification operability  
*       On March 18, 2011, division 3 diesel generator monthly surveillance
*       On March 20-21, 2011, functional checks with reactor core isolation cooling
*  
        valves at the remote shutdown panel
Test equipment removal  
Specific documents reviewed during this inspection are listed in the attachment.
                                    - 21 -                              Enclosure
*  
Restoration of plant systems  
*  
Updating of performance indicator data  
*  
Engineering evaluations, root causes, and bases for returning tested systems,  
structures, and components not meeting the test acceptance criteria were correct  
*  
Reference setting data  
*  
Annunciators and alarms setpoints  
The inspectors also verified that licensee personnel identified and implemented any  
needed corrective actions associated with the surveillance testing.
*  
On January 7, 2011, reactor coolant system leakage detection surveillance
*  
On February 4, 2011, inservice test of residual heat removal system B quarterly  
*  
On February 23, 2011, reactor coolant routine chemistry surveillance  
*  
On March 2, 2011, fuel handling area ventilation exhaust radiation monitor time  
response test  
*  
On March 10, 2011, division 1 diesel generator monthly surveillance  
*  
On March 18, 2011, division 3 diesel generator monthly surveillance  
*  
On March 20-21, 2011, functional checks with reactor core isolation cooling  
valves at the remote shutdown panel  
Specific documents reviewed during this inspection are listed in the attachment.  


      These activities constitute completion of seven surveillance (one reactor coolant system
      leakage detection, one inservice test, and five routine tests) testing inspection samples
      as defined in Inspection Procedure 71111.22-05.
- 22 -
  b. Findings
Enclosure
      No findings were identified.
These activities constitute completion of seven surveillance (one reactor coolant system  
      Cornerstone: Emergency Preparedness
leakage detection, one inservice test, and five routine tests) testing inspection samples  
1EP6 Drill Evaluation (71114.06)
as defined in Inspection Procedure 71111.22-05.  
.1   Emergency Preparedness Drill Observation
  a. Inspection Scope
b.  
      The inspectors evaluated the conduct of a routine licensee emergency drill on March 3,
No findings were identified.
      2011, to identify any weaknesses and deficiencies in classification, notification, and
Findings
      protective action recommendation development activities. The inspectors observed
      emergency response operations in the simulator control room and emergency
Cornerstone: Emergency Preparedness  
      operations facility to determine whether the event classification, notifications, and
1EP6 Drill Evaluation (71114.06)  
      protective action recommendations were performed in accordance with procedures. The
.1  
      inspectors also attended the licensee drill critique to compare any inspector-observed
Emergency Preparedness Drill Observation  
      weakness with those identified by the licensee staff in order to evaluate the critique and
a.  
      to verify whether the licensee staff was properly identifying weaknesses and entering
The inspectors evaluated the conduct of a routine licensee emergency drill on March 3,  
      them into the corrective action program. As part of the inspection, the inspectors
2011, to identify any weaknesses and deficiencies in classification, notification, and  
      reviewed the drill package and other documents listed in the attachment.
protective action recommendation development activities. The inspectors observed  
      These activities constitute completion of one sample as defined in Inspection
emergency response operations in the simulator control room and emergency  
      Procedure 71114.06-05.
operations facility to determine whether the event classification, notifications, and  
  b. Findings
protective action recommendations were performed in accordance with procedures. The  
      No findings were identified.
inspectors also attended the licensee drill critique to compare any inspector-observed  
2.   RADIATION SAFETY
weakness with those identified by the licensee staff in order to evaluate the critique and  
      Cornerstone: Occupational and Public Radiation Safety
to verify whether the licensee staff was properly identifying weaknesses and entering  
2RS01 Radiological Hazard Assessment and Exposure Controls (71124.01)
them into the corrective action program. As part of the inspection, the inspectors  
  a. Inspection Scope
reviewed the drill package and other documents listed in the attachment.  
      This area was inspected to: (1) review and assess licensees performance in assessing
Inspection Scope
      the radiological hazards in the workplace associated with licensed activities and the
      implementation of appropriate radiation monitoring and exposure control measures for
These activities constitute completion of one sample as defined in Inspection  
      both individual and collective exposures, (2) verify the licensee is properly identifying
Procedure 71114.06-05.  
      and reporting Occupational Radiation Safety Cornerstone performance indicators, and
                                          - 22 -                                Enclosure
b.  
No findings were identified.  
Findings
2.  
RADIATION SAFETY  
Cornerstone: Occupational and Public Radiation Safety  
2RS01 Radiological Hazard Assessment and Exposure Controls (71124.01)  
a.  
Inspection Scope  
This area was inspected to: (1) review and assess licensees performance in assessing  
the radiological hazards in the workplace associated with licensed activities and the  
implementation of appropriate radiation monitoring and exposure control measures for  
both individual and collective exposures, (2) verify the licensee is properly identifying  
and reporting Occupational Radiation Safety Cornerstone performance indicators, and  


  (3) identify those performance deficiencies that were reportable as a performance
  indicator and which may have represented a substantial potential for overexposure of
  the worker.
- 23 -
  The inspectors used the requirements in 10 CFR Part 20, the technical specifications,
Enclosure
  and the licensees procedures required by technical specifications as criteria for
(3) identify those performance deficiencies that were reportable as a performance  
  determining compliance. During the inspection, the inspectors interviewed the radiation
indicator and which may have represented a substantial potential for overexposure of  
  protection manager, radiation protection supervisors, and radiation workers. The
the worker.  
  inspectors performed walkdowns of various portions of the plant, performed independent
  radiation dose rate measurements and reviewed the following items:
The inspectors used the requirements in 10 CFR Part 20, the technical specifications,  
  *       Performance indicator events and associated documentation reported by the
and the licensees procedures required by technical specifications as criteria for  
          licensee in the Occupational Radiation Safety Cornerstone
determining compliance. During the inspection, the inspectors interviewed the radiation  
  *       The hazard assessment program, including a review of the licenses evaluations
protection manager, radiation protection supervisors, and radiation workers. The  
          of changes in plant operations and radiological surveys to detect dose rates,
inspectors performed walkdowns of various portions of the plant, performed independent  
          airborne radioactivity, and surface contamination levels
radiation dose rate measurements and reviewed the following items:  
  *       Instructions and notices to workers, including labeling or marking containers of
          radioactive material, radiation work permits, actions for electronic dosimeter
*  
          alarms, and changes to radiological conditions
Performance indicator events and associated documentation reported by the  
  *       Programs and processes for control of sealed sources and release of potentially
licensee in the Occupational Radiation Safety Cornerstone  
          contaminated material from the radiologically controlled area, including survey
          performance, instrument sensitivity, release criteria, procedural guidance, and
*  
          sealed source accountability
The hazard assessment program, including a review of the licenses evaluations  
  *       Radiological hazards control and work coverage, including the adequacy of
of changes in plant operations and radiological surveys to detect dose rates,  
          surveys, radiation protection job coverage, and contamination controls; the use of
airborne radioactivity, and surface contamination levels  
          electronic dosimeters in high noise areas; dosimetry placement; airborne
          radioactivity monitoring; controls for highly activated or contaminated materials
*  
          (non-fuel) stored within spent fuel and other storage pools; and posting and
Instructions and notices to workers, including labeling or marking containers of  
          physical controls for high radiation areas and very high radiation areas
radioactive material, radiation work permits, actions for electronic dosimeter  
  *       Radiation worker and radiation protection technician performance with respect to
alarms, and changes to radiological conditions  
          radiation protection work requirements
  *       Audits, self-assessments, and corrective action documents related to radiological
*  
          hazard assessment and exposure controls since the last inspection
Programs and processes for control of sealed sources and release of potentially  
  Specific documents reviewed during this inspection are listed in the attachment.
contaminated material from the radiologically controlled area, including survey  
  These activities constitute completion of the one required sample as defined in
performance, instrument sensitivity, release criteria, procedural guidance, and  
  Inspection Procedure 71124.01-05.
sealed source accountability  
b. Findings
                                        - 23 -                                Enclosure
*  
Radiological hazards control and work coverage, including the adequacy of  
surveys, radiation protection job coverage, and contamination controls; the use of  
electronic dosimeters in high noise areas; dosimetry placement; airborne  
radioactivity monitoring; controls for highly activated or contaminated materials  
(non-fuel) stored within spent fuel and other storage pools; and posting and  
physical controls for high radiation areas and very high radiation areas  
*  
Radiation worker and radiation protection technician performance with respect to  
radiation protection work requirements  
*  
Audits, self-assessments, and corrective action documents related to radiological  
hazard assessment and exposure controls since the last inspection  
Specific documents reviewed during this inspection are listed in the attachment.  
These activities constitute completion of the one required sample as defined in  
Inspection Procedure 71124.01-05.  
b.  
Findings  


Introduction. The inspectors identified a Green, noncited violation of Technical
Specification 5.7.2, resulting from the licensees failure to use a qualified radiation
protection technician to provide direct continuous coverage of work in a locked high
- 24 -
radiation area.
Enclosure
Description. The inspectors reviewed Condition Report CR-GGN-2011-00655, which
Introduction. The inspectors identified a Green, noncited violation of Technical  
documented the identification by Cooper Nuclear Station that a contractor seeking
Specification 5.7.2, resulting from the licensees failure to use a qualified radiation  
employment as a radiation protection technician did not meet ANSI 18.1 requirements.
protection technician to provide direct continuous coverage of work in a locked high  
The finding, documented February 2, 2011, was discussed with Entergy sites during a
radiation area.  
teleconference. Then, Grand Gulf Nuclear Station determined the individual had been
employed as a radiation protection technician at Grand Gulf Nuclear Station during
Description. The inspectors reviewed Condition Report CR-GGN-2011-00655, which  
Refueling Outage 17, conducted in April and May 2010. In response, Grand Gulf
documented the identification by Cooper Nuclear Station that a contractor seeking  
Nuclear Station reviewed the radiation surveys performed by the individual (from April 15
employment as a radiation protection technician did not meet ANSI 18.1 requirements.
through May 13, 2010), concluded the surveys contained data comparable with that
The finding, documented February 2, 2011, was discussed with Entergy sites during a  
documented in other surveys in the same areas under similar conditions, and closed the
teleconference. Then, Grand Gulf Nuclear Station determined the individual had been  
condition report on February 8, 2011. The inspectors reviewed the radiation survey
employed as a radiation protection technician at Grand Gulf Nuclear Station during  
records included in the condition report and noted something the licensee had not
Refueling Outage 17, conducted in April and May 2010. In response, Grand Gulf  
addressed. On April 27, 2010, the individual had provided job coverage for work in a
Nuclear Station reviewed the radiation surveys performed by the individual (from April 15  
locked high radiation area (an area with dose rates greater than 1000 mrem/hour).
through May 13, 2010), concluded the surveys contained data comparable with that  
Survey GG-1004-0660 identified the work area as the 128-foot auxiliary pipe chase,
documented in other surveys in the same areas under similar conditions, and closed the  
above the reactor water cleanup pump rooms. Since the individual used by the licensee
condition report on February 8, 2011. The inspectors reviewed the radiation survey  
to provide job coverage and surveillance in a locked high radiation area was not a
records included in the condition report and noted something the licensee had not  
qualified radiation protection technician, the inspectors identified this as a performance
addressed. On April 27, 2010, the individual had provided job coverage for work in a  
deficiency.
locked high radiation area (an area with dose rates greater than 1000 mrem/hour).  
Analysis. The failure to use a qualified radiation protection technician to provide direct
Survey GG-1004-0660 identified the work area as the 128-foot auxiliary pipe chase,  
continuous coverage of work in a locked high radiation area is a performance deficiency.
above the reactor water cleanup pump rooms. Since the individual used by the licensee  
The finding was more than minor because it was associated with the Occupational
to provide job coverage and surveillance in a locked high radiation area was not a  
Radiation Safety Cornerstone attribute (exposure control) of program and process and
qualified radiation protection technician, the inspectors identified this as a performance  
affected the cornerstone objective, in that, the failure to use qualified radiation protection
deficiency.  
technicians to provide job coverage in a high radiation area with dose rates in excess of
1000 mrem/hr had the potential to increase personnel dose. Using the Occupational
Analysis. The failure to use a qualified radiation protection technician to provide direct  
Radiation Safety Significance Determination Process, the inspectors determined the
continuous coverage of work in a locked high radiation area is a performance deficiency.
finding to have very low safety significance because: (1) it was not associated with
The finding was more than minor because it was associated with the Occupational  
ALARA planning or work controls, (2) there was no overexposure, (3) there was no
Radiation Safety Cornerstone attribute (exposure control) of program and process and  
substantial potential for an overexposure, and (4) the ability to assess dose was not
affected the cornerstone objective, in that, the failure to use qualified radiation protection  
compromised. The inspectors identified no cross-cutting aspect associated with this
technicians to provide job coverage in a high radiation area with dose rates in excess of  
finding.
1000 mrem/hr had the potential to increase personnel dose. Using the Occupational  
Enforcement. Technical Specification 5.7.2, controls for high radiation areas with dose
Radiation Safety Significance Determination Process, the inspectors determined the  
rates greater than 1000 mrem/hour, consists of all the controls for high radiation areas
finding to have very low safety significance because: (1) it was not associated with  
(Technical Specification 5.7.1) plus it requires doors to the area remain locked except
ALARA planning or work controls, (2) there was no overexposure, (3) there was no  
during periods of access by personnel under an approved radiation work permit that
substantial potential for an overexposure, and (4) the ability to assess dose was not  
shall specify the dose rate levels in the immediate work areas and the maximum
compromised.   The inspectors identified no cross-cutting aspect associated with this  
allowable stay times for individuals in those areas. In lieu of the stay time specification
finding.  
for the radiation work permit, direct or remote continuous surveillance may be made by
personnel qualified in radiation protection procedures to provide positive exposure
Enforcement. Technical Specification 5.7.2, controls for high radiation areas with dose  
                                    - 24 -                                Enclosure
rates greater than 1000 mrem/hour, consists of all the controls for high radiation areas  
(Technical Specification 5.7.1) plus it requires doors to the area remain locked except  
during periods of access by personnel under an approved radiation work permit that  
shall specify the dose rate levels in the immediate work areas and the maximum  
allowable stay times for individuals in those areas. In lieu of the stay time specification  
for the radiation work permit, direct or remote continuous surveillance may be made by  
personnel qualified in radiation protection procedures to provide positive exposure  


      control over the activities being performed within the area. Contrary to the above, during
      work in an area with dose rates greater than 1000 mrem/hour on April 27, 2010, in lieu of
      the stay time specification for the radiation work permit, direct or remote surveillance
- 25 -
      was not made by personnel qualified in radiation protection procedures to provide
Enclosure
      positive exposure control over the activities being performed within the area. Instead, an
control over the activities being performed within the area. Contrary to the above, during  
      unqualified person was assigned to provide surveillance of a locked high radiation on
work in an area with dose rates greater than 1000 mrem/hour on April 27, 2010, in lieu of  
      April 27, 2010. The licensee initiated Condition Report CR-GGN-2011-01045 to
the stay time specification for the radiation work permit, direct or remote surveillance  
      document the fact that it failed to identify this performance deficiency as part of the
was not made by personnel qualified in radiation protection procedures to provide  
      review associated with the closure of Condition Report CR-GGN-2011-00655.
positive exposure control over the activities being performed within the area. Instead, an  
      Because the violation was of very low safety significance and it was entered into the
unqualified person was assigned to provide surveillance of a locked high radiation on  
      licensees corrective action program, the violation is being treated as a noncited
April 27, 2010. The licensee initiated Condition Report CR-GGN-2011-01045 to  
      violation, consistent with the enforcement policy. NCV 05000416/2011002-04, Failure
document the fact that it failed to identify this performance deficiency as part of the  
      to Use a Qualified Radiation Protection Technician to Provide Direct Continuous
review associated with the closure of Condition Report CR-GGN-2011-00655.  
      Coverage of Work in a Locked High Radiation Area.
Because the violation was of very low safety significance and it was entered into the  
2RS02 Occupational ALARA Planning and Controls (71124.02)
licensees corrective action program, the violation is being treated as a noncited  
  a.  Inspection Scope
violation, consistent with the enforcement policy. NCV 05000416/2011002-04, Failure  
      This area was inspected to assess performance with respect to maintaining occupational
to Use a Qualified Radiation Protection Technician to Provide Direct Continuous  
      individual and collective radiation exposures as low as is reasonably achievable
Coverage of Work in a Locked High Radiation Area.  
      (ALARA). The inspectors used the requirements in 10 CFR Part 20, the technical
      specifications, and the licensees procedures required by technical specifications as
2RS02 Occupational ALARA Planning and Controls (71124.02)  
      criteria for determining compliance. During the inspection, the inspectors interviewed
      licensee personnel and reviewed the following items:
a.  
      *       Site-specific ALARA procedures and collective exposure history, including the
   
              current 3-year rolling average, site-specific trends in collective exposures, and
Inspection Scope  
              source-term measurements
This area was inspected to assess performance with respect to maintaining occupational  
      *       ALARA work activity evaluations/postjob reviews, exposure estimates, and
individual and collective radiation exposures as low as is reasonably achievable  
              exposure mitigation requirements
(ALARA). The inspectors used the requirements in 10 CFR Part 20, the technical  
      *       The methodology for estimating work activity exposures, the intended dose
specifications, and the licensees procedures required by technical specifications as  
              outcome, the accuracy of dose rate and man-hour estimates, and intended
criteria for determining compliance. During the inspection, the inspectors interviewed  
              versus actual work activity doses and the reasons for any inconsistencies
licensee personnel and reviewed the following items:  
      *       Records detailing the historical trends and current status of tracked plant source
              terms and contingency plans for expected changes in the source term due to
*  
              changes in plant fuel performance issues or changes in plant primary chemistry
Site-specific ALARA procedures and collective exposure history, including the  
      *       Radiation worker and radiation protection technician performance during work
current 3-year rolling average, site-specific trends in collective exposures, and  
              activities in radiation areas, airborne radioactivity areas, or high radiation areas
source-term measurements  
      *       Audits, self-assessments, and corrective action documents related to ALARA
              planning and controls since the last inspection
*  
                                            - 25 -                                Enclosure
ALARA work activity evaluations/postjob reviews, exposure estimates, and  
exposure mitigation requirements  
*  
The methodology for estimating work activity exposures, the intended dose  
outcome, the accuracy of dose rate and man-hour estimates, and intended  
versus actual work activity doses and the reasons for any inconsistencies  
*  
Records detailing the historical trends and current status of tracked plant source  
terms and contingency plans for expected changes in the source term due to  
changes in plant fuel performance issues or changes in plant primary chemistry  
*  
Radiation worker and radiation protection technician performance during work  
activities in radiation areas, airborne radioactivity areas, or high radiation areas  
*  
Audits, self-assessments, and corrective action documents related to ALARA  
planning and controls since the last inspection  


      Specific documents reviewed during this inspection are listed in the attachment.
      These activities constitute completion of the one required sample as defined in
      Inspection Procedure 71124.02-05.
- 26 -
  b. Findings
Enclosure
      No findings were identified.
Specific documents reviewed during this inspection are listed in the attachment.  
4.   OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
These activities constitute completion of the one required sample as defined in  
.1   Data Submission Issue
Inspection Procedure 71124.02-05.  
  a. Inspection Scope
      The inspectors performed a review of the performance indicator data submitted by the
b.  
      licensee for the fourth Quarter 2010 performance indicators for any obvious
      inconsistencies prior to its public release in accordance with Inspection Manual
Findings  
      Chapter 0608, Performance Indicator Program.
No findings were identified.  
      This review was performed as part of the inspectors normal plant status activities and,
4.  
      as such, did not constitute a separate inspection sample.
OTHER ACTIVITIES  
  b. Findings
4OA1 Performance Indicator Verification (71151)  
      No findings were identified.
.1  
.2   Unplanned Scrams per 7000 Critical Hours (IE01)
Data Submission Issue  
  a. Inspection Scope
a.  
      The inspectors sampled licensee submittals for the unplanned scrams per 7000 critical
The inspectors performed a review of the performance indicator data submitted by the  
      hours performance indicator for the period from the first quarter 2010 through the fourth
licensee for the fourth Quarter 2010 performance indicators for any obvious  
      quarter 2010. To determine the accuracy of the performance indicator data reported
inconsistencies prior to its public release in accordance with Inspection Manual  
      during those periods, the inspectors used definitions and guidance contained in NEI
Chapter 0608, Performance Indicator Program.  
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.
Inspection Scope
      The inspectors reviewed the licensees operator narrative logs, condition reports, event
      reports, and NRC integrated inspection reports for the period of January 2010 through
This review was performed as part of the inspectors normal plant status activities and,  
      December 2010 to validate the accuracy of the submittals. The inspectors also reviewed
as such, did not constitute a separate inspection sample.
      the licensees condition report database to determine if any problems had been identified
      with the performance indicator data collected or transmitted for this indicator and none
b.  
      were identified. Specific documents reviewed are described in the attachment to this
No findings were identified.
      report.
Findings
      These activities constitute completion of one unplanned scrams per 7000 critical hours
      sample as defined in Inspection Procedure 71151-05.
.2  
                                          - 26 -                              Enclosure
Unplanned Scrams per 7000 Critical Hours (IE01)  
a.  
The inspectors sampled licensee submittals for the unplanned scrams per 7000 critical  
hours performance indicator for the period from the first quarter 2010 through the fourth  
quarter 2010. To determine the accuracy of the performance indicator data reported  
during those periods, the inspectors used definitions and guidance contained in NEI  
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.
The inspectors reviewed the licensees operator narrative logs, condition reports, event  
reports, and NRC integrated inspection reports for the period of January 2010 through  
December 2010 to validate the accuracy of the submittals. The inspectors also reviewed  
the licensees condition report database to determine if any problems had been identified  
with the performance indicator data collected or transmitted for this indicator and none  
were identified. Specific documents reviewed are described in the attachment to this  
report.  
Inspection Scope
These activities constitute completion of one unplanned scrams per 7000 critical hours  
sample as defined in Inspection Procedure 71151-05.  


  b. Findings
      No findings were identified.
.3   Unplanned Scrams with Complications (IE02)
- 27 -
  a. Inspection Scope
Enclosure
      The inspectors sampled licensee submittals for the unplanned scrams with
      complications performance indicator for the period from first quarter 2010 through the
b.  
      fourth quarter 2010. To determine the accuracy of the performance indicator data
No findings were identified.  
      reported during those periods, the inspectors used definitions and guidance contained in
Findings
      NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,
      Revision 6. The inspectors reviewed the licensees operator narrative logs, condition
.3  
      reports, event reports, and NRC integrated inspection reports for the period of January
Unplanned Scrams with Complications (IE02)  
      2010 through December 2010 to validate the accuracy of the submittals. The inspectors
a.  
      also reviewed the licensees condition report database to determine if any problems had
The inspectors sampled licensee submittals for the unplanned scrams with  
      been identified with the performance indicator data collected or transmitted for this
complications performance indicator for the period from first quarter 2010 through the  
      indicator and none were identified. Specific documents reviewed are described in the
fourth quarter 2010. To determine the accuracy of the performance indicator data  
      attachment to this report.
reported during those periods, the inspectors used definitions and guidance contained in  
      These activities constitute completion of one unplanned scrams with complications
NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,  
      sample as defined in Inspection Procedure 71151-05.
Revision 6. The inspectors reviewed the licensees operator narrative logs, condition  
  b. Findings
reports, event reports, and NRC integrated inspection reports for the period of January  
      No findings were identified.
2010 through December 2010 to validate the accuracy of the submittals. The inspectors  
.4   Unplanned Power Changes per 7000 Critical Hours (IE03)
also reviewed the licensees condition report database to determine if any problems had  
  a. Inspection Scope
been identified with the performance indicator data collected or transmitted for this  
      The inspectors sampled licensee submittals for the unplanned power changes per 7000
indicator and none were identified. Specific documents reviewed are described in the  
      critical hours performance indicator for the period from first quarter 2010 through the
attachment to this report.  
      fourth quarter 2010. To determine the accuracy of the performance indicator data
Inspection Scope
      reported during those periods, the inspectors used definitions and guidance contained in
      NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,
These activities constitute completion of one unplanned scrams with complications  
      Revision 6. The inspectors reviewed the licensees operator narrative logs, condition
sample as defined in Inspection Procedure 71151-05.  
      reports, event reports, and NRC integrated inspection reports for the period of January
      2010 through December 2010 to validate the accuracy of the submittals. The inspectors
b.  
      also reviewed the licensees condition report database to determine if any problems had
No findings were identified.  
      been identified with the performance indicator data collected or transmitted for this
Findings
      indicator and none were identified. Specific documents reviewed are described in the
      attachment to this report.
.4  
      These activities constitute completion of one unplanned transients per 7000 critical
Unplanned Power Changes per 7000 Critical Hours (IE03)  
      hours sample as defined in Inspection Procedure 71151-05.
a.  
                                        - 27 -                                Enclosure
The inspectors sampled licensee submittals for the unplanned power changes per 7000  
critical hours performance indicator for the period from first quarter 2010 through the  
fourth quarter 2010. To determine the accuracy of the performance indicator data  
reported during those periods, the inspectors used definitions and guidance contained in  
NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,  
Revision 6. The inspectors reviewed the licensees operator narrative logs, condition  
reports, event reports, and NRC integrated inspection reports for the period of January  
2010 through December 2010 to validate the accuracy of the submittals. The inspectors  
also reviewed the licensees condition report database to determine if any problems had  
been identified with the performance indicator data collected or transmitted for this  
indicator and none were identified. Specific documents reviewed are described in the  
attachment to this report.  
Inspection Scope
These activities constitute completion of one unplanned transients per 7000 critical  
hours sample as defined in Inspection Procedure 71151-05.  


  b. Findings
      No findings were identified.
.5   Occupational Exposure Control Effectiveness (OR01)
- 28 -
  a. Inspection Scope
Enclosure
      The inspectors reviewed performance indicator data for the second quarter of 2010
      through the fourth quarter of 2010. The objective of the inspection was to determine the
b.  
      accuracy and completeness of the performance indicator data reported during these
No findings were identified.  
      periods. The inspectors used the definitions and clarifying notes contained in NEI
Findings
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,
      as criteria for determining whether the licensee was in compliance.
.5  
      The inspectors reviewed corrective action program records associated with high
Occupational Exposure Control Effectiveness (OR01)  
      radiation area (greater than 1 rem/hr) and very high radiation area non-conformances.
      The inspectors reviewed radiological, controlled area exit transactions greater than
a.  
      100 mrem. The inspectors also conducted walkdowns of high radiation areas (greater
      than 1 rem/hr) and very high radiation area entrances to determine the adequacy of the
Inspection Scope  
      controls of these areas.
The inspectors reviewed performance indicator data for the second quarter of 2010  
      These activities constitute completion of the occupational exposure control effectiveness
through the fourth quarter of 2010. The objective of the inspection was to determine the  
      sample as defined in Inspection Procedure 71151-05.
accuracy and completeness of the performance indicator data reported during these  
  b. Findings
periods. The inspectors used the definitions and clarifying notes contained in NEI  
      No findings were identified.
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,  
.6   Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual
as criteria for determining whether the licensee was in compliance.  
      Radiological Effluent Occurrences (PR01)
  a. Inspection Scope
The inspectors reviewed corrective action program records associated with high  
      The inspectors reviewed performance indicator data for the second quarter of 2010
radiation area (greater than 1 rem/hr) and very high radiation area non-conformances.
      through the fourth quarter of 2010. The objective of the inspection was to determine the
The inspectors reviewed radiological, controlled area exit transactions greater than  
      accuracy and completeness of the performance indicator data reported during these
100 mrem. The inspectors also conducted walkdowns of high radiation areas (greater  
      periods. The inspectors used the definitions and clarifying notes contained in NEI
than 1 rem/hr) and very high radiation area entrances to determine the adequacy of the  
      Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,
controls of these areas.  
      as criteria for determining whether the licensee was in compliance.
      The inspectors reviewed the licensees corrective action program records and selected
These activities constitute completion of the occupational exposure control effectiveness  
      individual annual or special reports to identify potential occurrences such as
sample as defined in Inspection Procedure 71151-05.  
      unmonitored, uncontrolled, or improperly calculated effluent releases that may have
      impacted offsite dose.
b.  
                                          - 28 -                                Enclosure
Findings  
No findings were identified.  
.6  
Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual  
Radiological Effluent Occurrences (PR01)  
a.  
Inspection Scope  
The inspectors reviewed performance indicator data for the second quarter of 2010  
through the fourth quarter of 2010. The objective of the inspection was to determine the  
accuracy and completeness of the performance indicator data reported during these  
periods. The inspectors used the definitions and clarifying notes contained in NEI  
Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,  
as criteria for determining whether the licensee was in compliance.  
The inspectors reviewed the licensees corrective action program records and selected  
individual annual or special reports to identify potential occurrences such as  
unmonitored, uncontrolled, or improperly calculated effluent releases that may have  
impacted offsite dose.  


      These activities constitute completion of the radiological effluent technical
      specifications/offsite dose calculation manual radiological effluent occurrences sample
      as defined in Inspection Procedure 71151-05.
- 29 -
  b. Findings
Enclosure
      No findings were identified.
These activities constitute completion of the radiological effluent technical  
4OA2 Identification and Resolution of Problems (71152)
specifications/offsite dose calculation manual radiological effluent occurrences sample  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
as defined in Inspection Procedure 71151-05.  
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
      Physical Protection
b.  
.1   Routine Review of Identification and Resolution of Problems
  a. Inspection Scope
Findings  
      As part of the various baseline inspection procedures discussed in previous sections of
No findings were identified.  
      this report, the inspectors routinely reviewed issues during baseline inspection activities
      and plant status reviews to verify that they were being entered into the licensees
4OA2 Identification and Resolution of Problems (71152)  
      corrective action program at an appropriate threshold, that adequate attention was being
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
      given to timely corrective actions, and that adverse trends were identified and
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and  
      addressed. The inspectors reviewed attributes that included the complete and accurate
Physical Protection  
      identification of the problem; the timely correction, commensurate with the safety
.1  
      significance; the evaluation and disposition of performance issues, generic implications,
Routine Review of Identification and Resolution of Problems  
      common causes, contributing factors, root causes, extent of condition reviews, and
a.  
      previous occurrences reviews; and the classification, prioritization, focus, and timeliness
As part of the various baseline inspection procedures discussed in previous sections of  
      of corrective actions. Minor issues entered into the licensees corrective action program
this report, the inspectors routinely reviewed issues during baseline inspection activities  
      because of the inspectors observations are included in the attached list of documents
and plant status reviews to verify that they were being entered into the licensees  
      reviewed.
corrective action program at an appropriate threshold, that adequate attention was being  
      These routine reviews for the identification and resolution of problems did not constitute
given to timely corrective actions, and that adverse trends were identified and  
      any additional inspection samples. Instead, by procedure, they were considered an
addressed. The inspectors reviewed attributes that included the complete and accurate  
      integral part of the inspections performed during the quarter and documented in
identification of the problem; the timely correction, commensurate with the safety  
      Section 1 of this report.
significance; the evaluation and disposition of performance issues, generic implications,  
  b. Findings
common causes, contributing factors, root causes, extent of condition reviews, and  
      No findings were identified.
previous occurrences reviews; and the classification, prioritization, focus, and timeliness  
.2   Daily Corrective Action Program Reviews
of corrective actions. Minor issues entered into the licensees corrective action program  
  a. Inspection Scope
because of the inspectors observations are included in the attached list of documents  
      In order to assist with the identification of repetitive equipment failures and specific
reviewed.  
      human performance issues for follow-up, the inspectors performed a daily screening of
Inspection Scope
                                            - 29 -                                Enclosure
These routine reviews for the identification and resolution of problems did not constitute  
any additional inspection samples. Instead, by procedure, they were considered an  
integral part of the inspections performed during the quarter and documented in  
Section 1 of this report.  
b.  
No findings were identified.  
Findings
.2  
Daily Corrective Action Program Reviews  
a.  
In order to assist with the identification of repetitive equipment failures and specific  
human performance issues for follow-up, the inspectors performed a daily screening of  
Inspection Scope


      items entered into the licensees corrective action program. The inspectors
      accomplished this through review of the stations daily corrective action documents.
      The inspectors performed these daily reviews as part of their daily plant status
- 30 -
      monitoring activities and, as such, did not constitute any separate inspection samples.
Enclosure
  b. Findings
items entered into the licensees corrective action program. The inspectors  
      No findings were identified.
accomplished this through review of the stations daily corrective action documents.  
.3   Selected Issue Follow-up Inspection
  a. Inspection Scope
The inspectors performed these daily reviews as part of their daily plant status  
      During a review of items entered in the licensees corrective action program, the
monitoring activities and, as such, did not constitute any separate inspection samples.  
      inspectors recognized CR-GGN- 2009-05879 a corrective action item documenting
      temperature switches for safety related ventilation system. The inspectors reviewed that
b.  
      item as described in Inspection Procedure 71152.02 to verify, in part, licensee evaluation
No findings were identified.  
      and disposition of operability and reportability issues; consideration of extent of condition
Findings
      and cause, generic implications, common cause, and previous occurrences;
      classification and prioritization of the problems resolution commensurate with the safety
.3  
      significance; and identification of corrective actions that were appropriately focused to
Selected Issue Follow-up Inspection  
      correct the problem.
a.  
      These activities constitute completion of one in-depth problem identification and
During a review of items entered in the licensees corrective action program, the  
      resolution sample as defined in Inspection Procedure 71152-05.
inspectors recognized CR-GGN- 2009-05879 a corrective action item documenting  
  b. Findings
temperature switches for safety related ventilation system. The inspectors reviewed that  
      No findings were identified.
item as described in Inspection Procedure 71152.02 to verify, in part, licensee evaluation  
4OA3 Event Follow-up (71153)
and disposition of operability and reportability issues; consideration of extent of condition  
.1   (Closed) LER 05000416/2010-002-00, Control Room Air Conditioning Inoperability -
and cause, generic implications, common cause, and previous occurrences;  
      Loss of Both Trains
classification and prioritization of the problems resolution commensurate with the safety  
  a. Inspection Scope
significance; and identification of corrective actions that were appropriately focused to  
      On October 14, 2010, while operating at approximately 100 percent power, the train B
correct the problem.  
      control room air conditioner subsystem tripped on low oil pressure while the train A
Inspection Scope
      control room air conditioner subsystem was out of service for maintenance. The control
      room temperature increased and actions were taken to maintain control room
These activities constitute completion of one in-depth problem identification and  
      temperatures below the technical specification limit of 90 degrees Fahrenheit. The two
resolution sample as defined in Inspection Procedure 71152-05.
      control room air conditioning subsystems were inoperable for 64 hours and 24 minutes
      until the train A control room air conditioner was declared operable.
b.  
      The three possible failure mechanisms that the licensee identified in their root cause
No findings were identified.  
      evaluation were 1) the intermittent failure of the low oil differential pressure switch, 2) the
Findings
                                            - 30 -                                Enclosure
4OA3 Event Follow-up (71153)  
.1  
(Closed) LER 05000416/2010-002-00, Control Room Air Conditioning Inoperability -  
Loss of Both Trains  
a.  
On October 14, 2010, while operating at approximately 100 percent power, the train B  
control room air conditioner subsystem tripped on low oil pressure while the train A  
control room air conditioner subsystem was out of service for maintenance. The control  
room temperature increased and actions were taken to maintain control room  
temperatures below the technical specification limit of 90 degrees Fahrenheit. The two  
control room air conditioning subsystems were inoperable for 64 hours and 24 minutes  
until the train A control room air conditioner was declared operable.  
Inspection Scope
The three possible failure mechanisms that the licensee identified in their root cause  
evaluation were 1) the intermittent failure of the low oil differential pressure switch, 2) the  


  intermittent failure of one or more loading/unloading mechanisms, and 3) one or more of
  the temperature control valves were in an open condition or in a more than desired open
  position. The licensee also identified a contributing cause of failure to exclude foreign
- 31 -
  material during maintenance activities on the train B control room air conditioner.
Enclosure
  Inspectors reviewed the circumstances surrounding the event, the licensees response
intermittent failure of one or more loading/unloading mechanisms, and 3) one or more of  
  to the event, and the licensees corrective actions to preclude repetition. Documents
the temperature control valves were in an open condition or in a more than desired open  
  reviewed as part of this inspection are listed in the attachment. The enforcement
position. The licensee also identified a contributing cause of failure to exclude foreign  
  aspects of this finding are discussed in this section and in Section 1R12. This LER is
material during maintenance activities on the train B control room air conditioner.
  closed.
Inspectors reviewed the circumstances surrounding the event, the licensees response  
b. Findings
to the event, and the licensees corrective actions to preclude repetition. Documents  
  Introduction. The inspectors reviewed a self-revealing, Green noncited violation of 10
reviewed as part of this inspection are listed in the attachment. The enforcement  
  CFR Part 50, Appendix B, Criterion XVI, Corrective Action, after the licensee failed to
aspects of this finding are discussed in this section and in Section 1R12. This LER is  
  determine the cause and prevent recurrence of a significant condition adverse to quality
closed.  
  associated with the train B control room air conditioner compressor tripping due to low oil
b.  
  pressure.
Findings  
  Description. On October 14, 2010, the train B control room air conditioner subsystem
Introduction. The inspectors reviewed a self-revealing, Green noncited violation of 10  
  tripped on low oil pressure while the train A control room air conditioner subsystem was
CFR Part 50, Appendix B, Criterion XVI, Corrective Action, after the licensee failed to  
  out of service for maintenance. The control room temperature increased, and actions
determine the cause and prevent recurrence of a significant condition adverse to quality  
  were taken to maintain control room temperatures below the technical specification limit
associated with the train B control room air conditioner compressor tripping due to low oil  
  of 90 degrees Fahrenheit. The licensee determined that the event (i.e., one subsystem
pressure.  
  inoperable and unavailable for maintenance while the other subsystem was inoperable
Description. On October 14, 2010, the train B control room air conditioner subsystem  
  due to a trip) was reportable to the NRC. The two control room air conditioning
tripped on low oil pressure while the train A control room air conditioner subsystem was  
  subsystems were inoperable for 64 hours and 24 minutes until the train A control room
out of service for maintenance. The control room temperature increased, and actions  
  air conditioner was declared operable. This was a significant condition because it
were taken to maintain control room temperatures below the technical specification limit  
  rendered technical specification required equipment inoperable.
of 90 degrees Fahrenheit. The licensee determined that the event (i.e., one subsystem  
  The licensees corrective actions to address the event involved performing a root cause
inoperable and unavailable for maintenance while the other subsystem was inoperable  
  evaluation. The licensee concluded that the three possible failure mechanisms were 1)
due to a trip) was reportable to the NRC. The two control room air conditioning  
  an intermittent failure of low oil differential pressure switch, 2) an intermittent failure of
subsystems were inoperable for 64 hours and 24 minutes until the train A control room  
  one or more loading/unloading mechanisms, and 3) failure of one or more thermal
air conditioner was declared operable. This was a significant condition because it  
  expansion valves. The licensee also concluded that a contributing cause of the event
rendered technical specification required equipment inoperable.  
  was the failure to exclude foreign material during maintenance activities of the system.
The licensees corrective actions to address the event involved performing a root cause  
  The licensee addressed each of the possible root causes, as well as the contributing
evaluation. The licensee concluded that the three possible failure mechanisms were 1)  
  cause, since a single root cause could not be determined. The corrective action for the
an intermittent failure of low oil differential pressure switch, 2) an intermittent failure of  
  three probable root causes included 1) ensuring that only original differential pressure
one or more loading/unloading mechanisms, and 3) failure of one or more thermal  
  switches are used (or a suitable equivalent) for replacement; 2) revising planned
expansion valves. The licensee also concluded that a contributing cause of the event  
  maintenance tasks to included instructions for the loader/unloader disassembly,
was the failure to exclude foreign material during maintenance activities of the system.
  inspection and reassembly; 3) revising tasks for compressor A and B rebuilds; and 4)
The licensee addressed each of the possible root causes, as well as the contributing  
  revising compressor preventative maintenance tasks to record the degree of superheat
cause, since a single root cause could not be determined. The corrective action for the  
  for each thermal expansion valve.
three probable root causes included 1) ensuring that only original differential pressure  
  Despite the corrective actions implemented by the licensee, the train B control room air
switches are used (or a suitable equivalent) for replacement; 2) revising planned  
  conditioner compressor again tripped on December 13, 2010, due to low oil pressure.
maintenance tasks to included instructions for the loader/unloader disassembly,  
  After this trip and upon further evaluation, the licensee performed an additional
inspection and reassembly; 3) revising tasks for compressor A and B rebuilds; and 4)  
  corrective action that installed an inline suction filter with smaller filtering diameter and
revising compressor preventative maintenance tasks to record the degree of superheat  
                                          - 31 -                                  Enclosure
for each thermal expansion valve.  
Despite the corrective actions implemented by the licensee, the train B control room air  
conditioner compressor again tripped on December 13, 2010, due to low oil pressure.
After this trip and upon further evaluation, the licensee performed an additional  
corrective action that installed an inline suction filter with smaller filtering diameter and  


larger surface area to remove foreign material from the system. The licensee also
modified the operator rounds to obtain daily readings of differential pressure across this
new filter and through calculation, determined a differential pressure necessary to
- 32 -
change the filter. The condition report that documented the December 13th event was
Enclosure
closed to the corrective actions associated with the October 14th compressor trip and the
larger surface area to remove foreign material from the system. The licensee also  
new corrective action associated with the newly installed in line suction filter.
modified the operator rounds to obtain daily readings of differential pressure across this  
The licensee entered this event into their corrective actions program as condition report
new filter and through calculation, determined a differential pressure necessary to  
CR-GGN-2010-07315. Since the use of the new inline suction filter, they have not had
change the filter. The condition report that documented the December 13th event was  
any additional trips of the control room air conditioning B. The April 2011 inspection
closed to the corrective actions associated with the October 14th compressor trip and the  
showed that the filter had reduced foreign material on the compressor suction strainer by
new corrective action associated with the newly installed in line suction filter.  
40 percent from the March 2011 inspection. Also in May 2011, the licensee plans to
The licensee entered this event into their corrective actions program as condition report  
boroscope the evaporation section of the air conditioner to search for any other foreign
CR-GGN-2010-07315. Since the use of the new inline suction filter, they have not had  
material.
any additional trips of the control room air conditioning B. The April 2011 inspection  
Analysis. The inspectors determined that the failure to take corrective actions to prevent
showed that the filter had reduced foreign material on the compressor suction strainer by  
recurrence of the train B control room air conditioner compressor tripping due to low oil
40 percent from the March 2011 inspection. Also in May 2011, the licensee plans to  
pressure was a performance deficiency. This finding was more than minor because it
boroscope the evaporation section of the air conditioner to search for any other foreign  
was associated with the equipment performance attribute of the Mitigating Systems
material.  
Cornerstone and adversely affected the cornerstone objective to ensure the availability,
Analysis. The inspectors determined that the failure to take corrective actions to prevent  
reliability, and capability of systems that respond to initiating events to prevent
recurrence of the train B control room air conditioner compressor tripping due to low oil  
undesirable consequences. Using Inspection Manual Chapter 0609, "Significance
pressure was a performance deficiency. This finding was more than minor because it  
Determination Process," Phase 1 worksheets, the inspectors determined that a Phase 2
was associated with the equipment performance attribute of the Mitigating Systems  
estimate was required because the finding represented a loss of system safety function.
Cornerstone and adversely affected the cornerstone objective to ensure the availability,  
The plant-specific risk informed notebook does not include the evaluation of risk caused
reliability, and capability of systems that respond to initiating events to prevent  
by the loss of cooling to the main control room. Therefore, the senior reactor analyst
undesirable consequences. Using Inspection Manual Chapter 0609, "Significance  
conducted a Phase 3 analysis.
Determination Process," Phase 1 worksheets, the inspectors determined that a Phase 2  
The analyst noted that understanding the risk affect of control room chillers required a
estimate was required because the finding represented a loss of system safety function.
review of the following items:
The plant-specific risk informed notebook does not include the evaluation of risk caused  
    *   Loss of offsite power frequency (LOOP): Several alternative methods of cooling
by the loss of cooling to the main control room. Therefore, the senior reactor analyst  
          control room equipment are available provided offsite power is available.
conducted a Phase 3 analysis.  
          Therefore, the dominant risk impact of essential chillers is during a loss of offsite
The analyst noted that understanding the risk affect of control room chillers required a  
          power. The loss of offsite power frequency documented in the plant-specific
review of the following items:  
          SPAR model is 3.59 x 10-2/year.
*  
    *   Loss of the opposite train probability (PCH-A): The performance deficiency only
Loss of offsite power frequency (LOOP): Several alternative methods of cooling  
          affected Train B CRAC. Therefore, the Train A would still be available to cool the
control room equipment are available provided offsite power is available.
          main control room. The generic failure probability for a single train of safety-
Therefore, the dominant risk impact of essential chillers is during a loss of offsite  
          related equipment is approximately 3 x 10-2/demand.
power. The loss of offsite power frequency documented in the plant-specific  
    *   Exposure Period (EXP): Although the Train B CRAC system was placed in
SPAR model is 3.59 x 10-2/year.  
          service without correcting the failure mechanism on November 1, 2010, the
          chiller continued to be utilized and run for much of the time until failure on
*  
          December 13, 2010. The analyst noted that the chiller ran from November 12
Loss of the opposite train probability (PCH-A): The performance deficiency only  
          until it failed on December 13, 2010. Therefore, the time that the chiller was
affected Train B CRAC. Therefore, the Train A would still be available to cool the  
          actually unavailable to perform its 24-hour risk significant mission time was
main control room. The generic failure probability for a single train of safety-
                                        - 32 -                                Enclosure
related equipment is approximately 3 x 10-2/demand.  
*  
Exposure Period (EXP): Although the Train B CRAC system was placed in  
service without correcting the failure mechanism on November 1, 2010, the  
chiller continued to be utilized and run for much of the time until failure on  
December 13, 2010. The analyst noted that the chiller ran from November 12  
until it failed on December 13, 2010. Therefore, the time that the chiller was  
actually unavailable to perform its 24-hour risk significant mission time was  


              about 48 hours (the last 24 hours of its run and the 24 hours it took to repair).
              This gave an exposure time of 2 days.
          *   Conditional Core Damage Probability (CCDP): In the worst case failure of
- 33 -
              control room air conditioning would result in main control room abandonment.
Enclosure
              The generic CCDP for shutting the reactor down from outside the main control
about 48 hours (the last 24 hours of its run and the 24 hours it took to repair).
              room is approximately 0.1.
This gave an exposure time of 2 days.  
      The analyst determined that a bounding assessment of the change in core damage
      frequency (CDF), can be calculated as follows:
*  
              CDF = LOOP * PCH-A * EXP * CCDP
Conditional Core Damage Probability (CCDP): In the worst case failure of  
                      = 3.59 x 10-2/year * 3 x 10-2/demand * 2 days/365 days/year * 0.1
control room air conditioning would result in main control room abandonment.
                      = 5.9 x 10-7
The generic CCDP for shutting the reactor down from outside the main control  
      Based on the above bounding analysis, the analyst determined that the change in core
room is approximately 0.1.  
      damage frequency result was 5.9 x 10-7. This noncited violation was therefore
      determined to be of very low safety significance (Green). This finding had a crosscutting
The analyst determined that a bounding assessment of the change in core damage  
      aspect in the area of problem identification and resolution associated with the corrective
frequency (CDF), can be calculated as follows:  
      action program component because licensee personnel failed to thoroughly evaluate the
      multiple failures of the train B control room air conditioner compressor. [P.1(c)]
CDF = LOOP * PCH-A * EXP * CCDP  
      Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,
      states, in part, that in the case of a significant condition adverse to quality, measures
      shall assure that the cause of the condition is determined and corrective action taken to
= 3.59 x 10-2/year * 3 x 10-2/demand * 2 days/365 days/year * 0.1  
      preclude repetition. Contrary to the above, plant personnel did not implement corrective
      actions to preclude repetition of a significant condition adverse to quality associated with
      the tripping of the train B control room air conditioning compressor due to low oil
= 5.9 x 10-7  
      pressure. Specifically, on December 13, 2010, the train B control room air conditioner
      compressor tripped due to low oil pressure after the licensee had a performed a root
Based on the above bounding analysis, the analyst determined that the change in core  
      cause analysis to identify the cause and prevent recurrence of the compressor tripping
damage frequency result was 5.9 x 10-7. This noncited violation was therefore  
      due to low oil pressure. Because the finding was of very low safety significance and has
determined to be of very low safety significance (Green). This finding had a crosscutting  
      been entered into the corrective action program as Condition Report CR-GGN-2010-
aspect in the area of problem identification and resolution associated with the corrective  
      07315, this violation is being treated as a noncited violation, consistent with the NRC
action program component because licensee personnel failed to thoroughly evaluate the  
      Enforcement Policy. NCV 05000416/2011002-05, Failure to Prevent Recurrence of
multiple failures of the train B control room air conditioner compressor. [P.1(c)]  
      Control Room Air Conditioner Compressor Tripping Due to Low Oil Pressure.
Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,  
.2     Steam Leak in the Containment
states, in part, that in the case of a significant condition adverse to quality, measures  
  a. Inspection Scope
shall assure that the cause of the condition is determined and corrective action taken to  
      On November 8, 2010, the inspectors responded to the control room to observe operator
preclude repetition. Contrary to the above, plant personnel did not implement corrective  
      response to a steam leak in containment. The newly installed mitigation monitoring
actions to preclude repetition of a significant condition adverse to quality associated with  
      system positive displacement pump ejected the cylinder causing an approximate seven
the tripping of the train B control room air conditioning compressor due to low oil  
      gallons per minute reactor coolant leak. The inspectors observed operator actions,
pressure. Specifically, on December 13, 2010, the train B control room air conditioner  
      control room briefs and overall plant response to the event. The inspectors also
compressor tripped due to low oil pressure after the licensee had a performed a root  
                                            - 33 -                                Enclosure
cause analysis to identify the cause and prevent recurrence of the compressor tripping  
due to low oil pressure. Because the finding was of very low safety significance and has  
been entered into the corrective action program as Condition Report CR-GGN-2010-
07315, this violation is being treated as a noncited violation, consistent with the NRC  
Enforcement Policy. NCV 05000416/2011002-05, Failure to Prevent Recurrence of  
Control Room Air Conditioner Compressor Tripping Due to Low Oil Pressure.  
.2  
Steam Leak in the Containment
a.  
On November 8, 2010, the inspectors responded to the control room to observe operator  
response to a steam leak in containment. The newly installed mitigation monitoring  
system positive displacement pump ejected the cylinder causing an approximate seven  
gallons per minute reactor coolant leak. The inspectors observed operator actions,  
control room briefs and overall plant response to the event. The inspectors also  
Inspection Scope


  observed control room indications used to identify abnormal conditions in the
  containment building. Documents reviewed for this inspection are listed in the
  attachment.
- 34 -
b.  Findings
Enclosure
  Introduction. The inspectors reviewed a self-revealing, Green finding of EN-DC-115,
observed control room indications used to identify abnormal conditions in the  
  Engineering Change Process, involving the failure to maintain adequate design control
containment building. Documents reviewed for this inspection are listed in the  
  measures associated with the installation of the mitigation monitoring system.
attachment.
  Description. On November 8, 2010, at approximately 5:30 am, a reactor coolant
  pressure boundary failure occurred at the skid mounted Online Noble Chemical -
b.     Findings
  Mitigation Monitoring System pump inside primary containment. The positive
   
  displacement sample pump ejected the pump piston from the housing resulting in an
 
  approximate 7 gpm leak of reactor coolant. The leak was not detected for approximately
Introduction. The inspectors reviewed a self-revealing, Green finding of EN-DC-115,  
  4.5 hours, resulting in the release of approximately 2,000 gallons of reactor coolant
Engineering Change Process, involving the failure to maintain adequate design control  
  which flashed directly to steam. The steam leak resulted in a reactor recirculation system
measures associated with the installation of the mitigation monitoring system.  
  flow control valve lockup (due to HPU motor failure) and approximately 15,000 square
Description. On November 8, 2010, at approximately 5:30 am, a reactor coolant  
  feet of contaminated area in the primary containment structure.
pressure boundary failure occurred at the skid mounted Online Noble Chemical -  
  The inspectors reviewed the mitigation monitoring system modification documentation
Mitigation Monitoring System pump inside primary containment. The positive  
  and found that the design documentation did not appropriately address the design
displacement sample pump ejected the pump piston from the housing resulting in an  
  requirements for the installation of the mitigation monitoring system pump. The licensee
approximate 7 gpm leak of reactor coolant. The leak was not detected for approximately  
  failed to ensure proper validation testing for the pump prior to installation in the plant.
4.5 hours, resulting in the release of approximately 2,000 gallons of reactor coolant  
  Specifically, they did not ensure that the pump would be able to withstand the system
which flashed directly to steam. The steam leak resulted in a reactor recirculation system  
  operating pressures and temperatures in which it was installed. They failed to validate
flow control valve lockup (due to HPU motor failure) and approximately 15,000 square  
  the design, which had a single point vulnerability, that resulted in the piston injecting
feet of contaminated area in the primary containment structure.  
  from the pump and caused the leakage and contamination of the containment. In
The inspectors reviewed the mitigation monitoring system modification documentation  
  addition, the inspectors reviewed the root cause analysis of the event and found that the
and found that the design documentation did not appropriately address the design  
  licensee failed to apply the appropriate oversight of the engineering vendor due to
requirements for the installation of the mitigation monitoring system pump. The licensee  
  weaknesses in the procedure EN-DC-114, "Vendor Quality Management/Oversight."
failed to ensure proper validation testing for the pump prior to installation in the plant.
  The licensee entered this event into their corrective actions program as condition report
Specifically, they did not ensure that the pump would be able to withstand the system  
  CR-GGN-2010-07852. The licensee has currently removed the mitigation monitoring
operating pressures and temperatures in which it was installed. They failed to validate  
  system pump from the plant, and isolated the mitigation monitoring system skid from the
the design, which had a single point vulnerability, that resulted in the piston injecting  
  reactor water cleanup system. They are evaluating the design to make appropriate
from the pump and caused the leakage and contamination of the containment. In  
  changes to ensure a repeat of this event will not occur.
addition, the inspectors reviewed the root cause analysis of the event and found that the  
  Analysis. The failure to implement adequate design control measures for modifications
licensee failed to apply the appropriate oversight of the engineering vendor due to  
  to the plant, which impacted the reactor coolant pressure boundary, is a performance
weaknesses in the procedure EN-DC-114, "Vendor Quality Management/Oversight."  
  deficiency. Specifically procedure EN-DC-115, Engineering Change Process, step
The licensee entered this event into their corrective actions program as condition report  
  5.1[1], requires during the engineering change development a choice of new technology
CR-GGN-2010-07852. The licensee has currently removed the mitigation monitoring  
  or application is an error precursor which will need to have defensive functions built into
system pump from the plant, and isolated the mitigation monitoring system skid from the  
  the design, testing and maintenance, including developing in-house expertise. Contrary
reactor water cleanup system. They are evaluating the design to make appropriate  
  to this, the engineering change package that implemented this design change failed to
changes to ensure a repeat of this event will not occur.  
  ensure proper validation testing was performed prior to installation in the plant. The
Analysis. The failure to implement adequate design control measures for modifications  
  finding is more than minor because it affects the design control attribute of the Barrier
to the plant, which impacted the reactor coolant pressure boundary, is a performance  
  Integrity Cornerstone to provide reasonable assurance that physical design barriers
deficiency. Specifically procedure EN-DC-115, Engineering Change Process, step  
                                        - 34 -                                Enclosure
5.1[1], requires during the engineering change development a choice of new technology  
or application is an error precursor which will need to have defensive functions built into  
the design, testing and maintenance, including developing in-house expertise. Contrary  
to this, the engineering change package that implemented this design change failed to  
ensure proper validation testing was performed prior to installation in the plant. The  
finding is more than minor because it affects the design control attribute of the Barrier  
Integrity Cornerstone to provide reasonable assurance that physical design barriers  


      protect the public from radionuclide releases caused by accidents or events. Therefore,
      using inspection Manual Chapter 0609, "Significance Determination Process," Phase 1
      Worksheet for LOCA initiators, the inspectors concluded that the finding was of very low
- 35 -
      safety significance (Green) because the failure of the mitigation monitoring system would
Enclosure
      not have exceeded technical specifications limits for identified leakage in the reactor
protect the public from radionuclide releases caused by accidents or events. Therefore,  
      coolant system. This finding has a crosscutting aspect in the area of human
using inspection Manual Chapter 0609, "Significance Determination Process," Phase 1  
      performance associated with the work practices component because the licensee failed
Worksheet for LOCA initiators, the inspectors concluded that the finding was of very low  
      to adequately oversee the design of the mitigation monitor system such that nuclear
safety significance (Green) because the failure of the mitigation monitoring system would  
      safety is supported. [H.4(c)]
not have exceeded technical specifications limits for identified leakage in the reactor  
      Enforcement. No violation of regulatory requirements occurred. This finding was
coolant system. This finding has a crosscutting aspect in the area of human  
      entered into the licensees corrective action program as CR-GGN-2010-07852, and is
performance associated with the work practices component because the licensee failed  
      identified as: FIN 05000416/2011002-06, Inadequate Design Control for the Mitigation
to adequately oversee the design of the mitigation monitor system such that nuclear  
      Monitoring System Modification.
safety is supported. [H.4(c)]  
4OA5 Other Activities
Enforcement. No violation of regulatory requirements occurred. This finding was  
1.     (Closed) Temporary Instruction (TI) 2515/179, Verification of Licensee Responses to
entered into the licensees corrective action program as CR-GGN-2010-07852, and is  
      NRC Requirement for Inventories of Materials Tracked in the National Source Tracking
identified as: FIN 05000416/2011002-06, Inadequate Design Control for the Mitigation  
      System Pursuant to Title 10, Code of Federal Regulations, Part 20.2207 (10 CFR
Monitoring System Modification.  
      20.2207)
4OA5 Other Activities  
  a. Inspection Scope
1.
      An NRC inspection was performed to confirm that the licensee has reported their initial
(Closed) Temporary Instruction (TI) 2515/179, Verification of Licensee Responses to  
      inventories of sealed sources pursuant to 10 CFR 20.2207 and to verify that the National
NRC Requirement for Inventories of Materials Tracked in the National Source Tracking  
      Source Tracking System database correctly reflects the Category 1 and 2 sealed
System Pursuant to Title 10, Code of Federal Regulations, Part 20.2207 (10 CFR  
      sources in custody of the licensee. Inspectors interviewed personnel and performed the
20.2207)
      following:
      *     Reviewed the licensees source inventory
a.  
      *     Verified the presence of any Category 1 or 2 sources
Inspection Scope  
      *     Reviewed procedures for and evaluated the effectiveness of storage and handling
            of sources
An NRC inspection was performed to confirm that the licensee has reported their initial  
      *     Reviewed documents involving transactions of sources
inventories of sealed sources pursuant to 10 CFR 20.2207 and to verify that the National  
      *     Reviewed adequacy of licensee maintenance, posting, and labeling of nationally
Source Tracking System database correctly reflects the Category 1 and 2 sealed  
            tracked sources
sources in custody of the licensee. Inspectors interviewed personnel and performed the  
  b.  Findings
following:  
      While comparing the National Source Tracking System database information, the
*  
      Licensees information submittal, and original source certificates, the inspector noted
Reviewed the licensees source inventory
      that the licensee erroneously reported information for one of the four sources meeting
      the reporting criteria. The licensee used original leak test data and submitted the wrong
*  
                                          - 35 -                                Enclosure
Verified the presence of any Category 1 or 2 sources
*  
Reviewed procedures for and evaluated the effectiveness of storage and handling  
of sources  
*  
Reviewed documents involving transactions of sources  
*  
Reviewed adequacy of licensee maintenance, posting, and labeling of nationally  
tracked sources  
b.  
   
Findings  
While comparing the National Source Tracking System database information, the  
Licensees information submittal, and original source certificates, the inspector noted  
that the licensee erroneously reported information for one of the four sources meeting  
the reporting criteria. The licensee used original leak test data and submitted the wrong  


        serial number and activity date for the source. The licensee reviewed all relevant data
        and submitted corrected documents within the five business days allowed by
        10 CFR 20.2207(g). This finding was considered as an administrative error and of minor
- 36 -
        safety significance.
Enclosure
4OA6 Meetings
serial number and activity date for the source. The licensee reviewed all relevant data  
Exit Meeting Summary
and submitted corrected documents within the five business days allowed by  
On February 18, 2011, the inspectors presented the results of the radiation safety inspections to
10 CFR 20.2207(g). This finding was considered as an administrative error and of minor  
Mr. J. Browning, General Plant Manager, and other members of the licensee staff. The licensee
safety significance.  
acknowledged the issues presented. The inspectors asked the licensee whether any materials
examined during the inspection should be considered proprietary. No proprietary information
4OA6 Meetings  
was identified.
Exit Meeting Summary  
On February 18, 2011, the inspectors presented the results of the radiation safety inspections to  
Mr. J. Browning, General Plant Manager, and other members of the licensee staff. The licensee  
acknowledged the issues presented. The inspectors asked the licensee whether any materials  
examined during the inspection should be considered proprietary. No proprietary information  
was identified.  
On April 14, 2011, the inspectors presented the inspection results to M. Perito, Site Vice-
On April 14, 2011, the inspectors presented the inspection results to M. Perito, Site Vice-
President Operations and other members of the licensee staff. The licensee acknowledged the
President Operations and other members of the licensee staff. The licensee acknowledged the  
issues presented. The inspector asked the licensee whether any materials examined during the
issues presented. The inspector asked the licensee whether any materials examined during the  
inspection should be considered proprietary. No proprietary information was identified.
inspection should be considered proprietary. No proprietary information was identified.  
4OA7 Licensee-Identified Violations
The following violations of very low safety significance (Green) were identified by the licensee
4OA7 Licensee-Identified Violations  
and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC
The following violations of very low safety significance (Green) were identified by the licensee  
Enforcement Policy for being dispositioned as noncited violations.
and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC  
.1     Technical Requirements Manual (TRM) section 6.2.1 requires that fire detection
Enforcement Policy for being dispositioned as noncited violations.  
        instrumentation for each fire detection zone shall be operable and if the required
        detection system is inoperable an hourly fire watch must be established. Contrary to
.1  
        this, on February 9, 2011 the licensee identified that fire detection instrumentation for fire
Technical Requirements Manual (TRM) section 6.2.1 requires that fire detection  
        zone 2-12 had been left in the non-audible alarm for the main control room on the fire
instrumentation for each fire detection zone shall be operable and if the required  
        computer when the limiting condition for operations was cleared on December 8, 2010
detection system is inoperable an hourly fire watch must be established. Contrary to  
        when zone was returned to operable status. The control room supervisor on February 9,
this, on February 9, 2011 the licensee identified that fire detection instrumentation for fire  
        2011, discovered this condition when entering a fire-limiting condition for operation for
zone 2-12 had been left in the non-audible alarm for the main control room on the fire  
        the division 1 diesel generator room to allow welding. The licensee determined that it
computer when the limiting condition for operations was cleared on December 8, 2010  
        had been in non-audible status from December 8, 2010, through February 9, 2011. This
when zone was returned to operable status. The control room supervisor on February 9,  
        issue was documented in the licensees corrective action program in condition report
2011, discovered this condition when entering a fire-limiting condition for operation for  
        CR-GGN-2011-00851. The senior reactor analyst from region IV performed a bounding
the division 1 diesel generator room to allow welding. The licensee determined that it  
        evaluation of the change in risk caused by this condition. According to the Grand Gulf
had been in non-audible status from December 8, 2010, through February 9, 2011. This  
        Updated Final Safety Analysis Report, Fire Zone 2-12 only contains Division I
issue was documented in the licensees corrective action program in condition report  
        equipment. A fire that consumed the equipment in the area could not result in a loss of
CR-GGN-2011-00851. The senior reactor analyst from region IV performed a bounding  
        offsite power or other unplanned transient. Given the ignition frequency of the area, the
evaluation of the change in risk caused by this condition. According to the Grand Gulf  
        60-day exposure period, and the conditional core damage probability with the loss of the
Updated Final Safety Analysis Report, Fire Zone 2-12 only contains Division I  
        Division I emergency diesel generator, the analyst calculated that the change in risk was
equipment. A fire that consumed the equipment in the area could not result in a loss of  
        significantly less than 1E-6. Therefore, this finding was of very low safety significance
offsite power or other unplanned transient. Given the ignition frequency of the area, the  
        (Green).
60-day exposure period, and the conditional core damage probability with the loss of the  
                                            - 36 -                                  Enclosure
Division I emergency diesel generator, the analyst calculated that the change in risk was  
significantly less than 1E-6. Therefore, this finding was of very low safety significance  
(Green).  


- 37 - Enclosure
                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
- 37 -  
Licensee Personnel
Enclosure  
R. Benson, Manager (Acting), Radiation Protection
J. Browning, General Plant Manager
D. Coulter, Senior Licensing Specialist
H Farris, Assistant Operation Manager
K. Higgenbotham, Planning and Scheduling Manager
J. Houston, Maintenance Manager
R. Jackson, Licensing
C. Lewis, Manager, Emergency Preparedness
C. Perino, Licensing Manager
M. Perito, Site Vice President of Operations
M. Richey, Director, Nuclear Safety Assurance
F. Rosser, Supervisor, Dosimetry
R. Sumrall, Superintendant, Operations Training
R. Sylvan, Supervisor, Radiation Protection
T. Trichell, Radiation Protection Manager
D. Wiles, Engineering Director
R. Wilson, Manager, Quality Assurance
E. Wright, Supervisor, Radiation Protection
NRC Personnel
R. Smith, Senior Resident Inspector
                                          A-1            Attachment


                  LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
  Opened and Closed
   
                            Transient Combustible Stored in the Fire Exclusion Zone Near the
A-1
  05000416/2011002-01 NCV
   
                            Independent Spent Fuel Storage Installation (Section 1R05)
                            Failure to Update Available Low Pressure Coolant Injection Loops
  05000416/2011002-02 NCV
   
                            in the Updated Final Safety Analysis Report (Section 1R12)
Attachment
                            Failure to Demonstrate Maintenance Effectiveness of Train B
SUPPLEMENTAL INFORMATION
  05000416/2011002-03 NCV
KEY POINTS OF CONTACT 
                            Control Room Air Conditioner(Section 1R12)
                            Failure to Use a Qualified Radiation Protection Technician to
Licensee Personnel 
  05000416/2011002-04 NCV    Provide Direct Continuous Coverage of Work in a Locked High
   
                            Radiation Area (Section 2RS01)
R. Benson, Manager (Acting), Radiation Protection   
                            Failure to Prevent Recurrence of Control Room Air Conditioner
J. Browning, General Plant Manager
05000416/2011002-05 NCV
D. Coulter, Senior Licensing Specialist
                            Compressor Tripping Due to Low Oil Pressure (Section 4OA3)
H Farris, Assistant Operation Manager
                            Inadequate Design Control for the Mitigation Monitoring System
K. Higgenbotham, Planning and Scheduling Manager
05000416/2011002-06 FIN
J. Houston, Maintenance Manager
                            Modification (Section 4OA3)
R. Jackson, Licensing
Closed
C. Lewis, Manager, Emergency Preparedness
                            Verification of Licensee Responses to NRC Requirement for
C. Perino, Licensing Manager
                            Inventories of Materials Tracked in the National Source Tracking
M. Perito, Site Vice President of Operations
TI 2515/179            TI
M. Richey, Director, Nuclear Safety Assurance
                            System Pursuant to Title 10, Code of Federal Regulations,
F. Rosser, Supervisor, Dosimetry
                            Part 20.2207 (10 CFR 20.2207) (Section 4OA5)
R. Sumrall, Superintendant, Operations Training
  05000416/2010-002-00 LER Control Room Air Conditioning Inoperability - Loss of Both Trains
R. Sylvan, Supervisor, Radiation Protection
                            (Section 4OA3)
T. Trichell, Radiation Protection Manager
                                        A-2                                  Attachment
D. Wiles, Engineering Director
R. Wilson, Manager, Quality Assurance
E. Wright, Supervisor, Radiation Protection
NRC Personnel
R. Smith, Senior Resident Inspector
   


                          LIST OF DOCUMENTS REVIEWED
Section 1RO1: Adverse Weather Protection
PROCEDURE
A-2
    NUMBER                                TITLE                      REVISION
ENS-EP-302      Severe Weather Response                                  11
05-1-02-VI-2    Hurricanes, Tornados, and Severe Weather                113
04-1-01-P41-1  Standby Service Water System                            133
04-1-01-N71-1  Circulating Water System                                  72
Attachment
04-1-03-A30-1  Cold Weather Protection                                   20
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED 
OTHER
    NUMBER                                TITLE                        DATE
Opened and Closed
                SSW Pump Discharge Temperatures                    January 6-10,
05000416/2011002-01 NCV Transient Combustible Stored in the Fire Exclusion Zone Near the
                                                                        2011
Independent Spent Fuel Storage Installation (Section 1R05)
WORK ORDER
05000416/2011002-02 NCV Failure to Update Available Low Pressure Coolant Injection Loops
WO 52233022
in the Updated Final Safety Analysis Report (Section 1R12)
Section 1RO4: Equipment Alignment
05000416/2011002-03 NCV Failure to Demonstrate Maintenance Effectiveness of Train B
PROCEDURE
Control Room Air Conditioner(Section 1R12)
    NUMBER                                TITLE                      REVISION
05000416/2011002-04 NCV
9.3-17 - 9.3-25 GG UFSAR                                                  3
Failure to Use a Qualified Radiation Protection Technician to
07-1-34-C41-   Standby Liquid Control Pump                              10
Provide Direct Continuous Coverage of Work in a Locked High
C001-1
Radiation Area (Section 2RS01)
04-1-01-C41-1  Standby Liquid Control System                           119
05000416/2011002-05 NCV Failure to Prevent Recurrence of Control Room Air Conditioner
04-1-01-P75-1  Standby Diesel Generator System                          88
Compressor Tripping Due to Low Oil Pressure (Section 4OA3)
04-1-01-P41-1  Standby Service Water System                            133
05000416/2011002-06 FIN
04-1-01-E12-1  System Operating Instructions Residual Heat Removal      137
Inadequate Design Control for the Mitigation Monitoring System
                System
Modification (Section 4OA3)
04-1-01-E12-1  Residual Heat Removal B                                  137
04-1-01-E12-1  Residual Heat Removal C                                  137
                                      A-3                          Attachment
Closed
    
  TI 2515/179
TI
Verification of Licensee Responses to NRC Requirement for
Inventories of Materials Tracked in the National Source Tracking
System Pursuant to Title 10, Code of Federal Regulations,
Part 20.2207 (10 CFR 20.2207) (Section 4OA5)
05000416/2010-002-00 LER Control Room Air Conditioning Inoperability - Loss of Both Trains
(Section 4OA3)


PROCEDURE
    NUMBER                                   TITLE                         REVISION
04-1-01-E12-1     Residual Heat Removal B Attachment IB                        137
A-3
04-1-01-E12-1     Residual Heat Removal B Attachment IIIB                      137
04-1-01-E12-1     Residual Heat Removal C Attachment IC                        137
04-1-01-E12-1     Residual Heat Removal B Attachment VB                        137
04-1-01-E12-1     Residual Heat Removal (Interface Valves) Attachment IIE      137
04-1-01-P41-1     Standby Service Water System Attachment IIB                  133
Attachment
04-1-01-P41-1     Standby Service Water System Attachment IIIB                  113
LIST OF DOCUMENTS REVIEWED
OTHER
    NUMBER                                    TITLE                            DATE
Section 1RO1:  Adverse Weather Protection
11-4568            Scaffolding Evaluation Request                          February 15,
                                                                                2001
PROCEDURE  
CALCULATION
NUMBER  
    NUMBER                                    TITLE                            DATE
TITLE  
9645              Diesel Generator Building Walls                          August 2,
REVISION  
                                                                                1976
ENS-EP-302
C-C400            SSW CT and Basin (Pump-House) Tornado and No            May 28, 1976
Severe Weather Response
                  Earthquake
11
C-0-100            Diesel Generator Bldg. Walls Tornado Wind Load W        August 2,
05-1-02-VI-2
                                                                                1976
Hurricanes, Tornados, and Severe Weather
WORK ORDER
113
WO 52256371                        WO 00260559                  WO 00259801
04-1-01-P41-1  
Section 1RO5: Fire Protection
Standby Service Water System
PROCEDURE
133
      NUMBER                                    TITLE                        REVISION
04-1-01-N71-1  
Fire Pre-Plan DG-03    Division II Diesel Generator Room                          3
Circulating Water System
9A-343 - 9A347        GG UFSAR
72
Fire Pre-Plan A-02    RHR A Pump Room 1A103                                      1
04-1-03-A30-1  
                                          A-4                              Attachment
Cold Weather Protection
20
OTHER
NUMBER
TITLE
DATE
SSW Pump Discharge Temperatures
January 6-10,
2011
WORK ORDER
WO 52233022
Section 1RO4:  Equipment Alignment
PROCEDURE
NUMBER
TITLE
REVISION
9.3-17 - 9.3-25
GG UFSAR
3
07-1-34-C41-
C001-1  
Standby Liquid Control Pump
10
04-1-01-C41-1  
Standby Liquid Control System
119
04-1-01-P75-1  
Standby Diesel Generator System  
88
04-1-01-P41-1  
Standby Service Water System  
133
04-1-01-E12-1
System Operating Instructions Residual Heat Removal
System
137
04-1-01-E12-1
Residual Heat Removal B
137
04-1-01-E12-1
Residual Heat Removal C
137


PROCEDURE
      NUMBER                                     TITLE                         REVISION
Fire Pre-Plan A-03    RCIC Pump Room 1A104                                          1
A-4
Fire Pre-Plan A-04     RHR B Pump Room 1A105                                        1
9A.5.2.2              Safe Shutdown Equipment
Appendix 9B            Fire Protection Program
CONDITION REPORT
CR-GGN-2011-00862                CR-GGN-2011-01939              CR-GGN-2011-00851
Attachment
CR-GGN-2011-00455
PROCEDURE  
Section 1RO6: Flood Protection Measures
NUMBER  
PROCEDURE
TITLE  
    NUMBER                                     TITLE                           REVISION /
REVISION  
                                                                                  DATE
04-1-01-E12-1  
9A-336 - 9A338    GG UFSAR
Residual Heat Removal B Attachment IB
9A.5.59            GG UFSAR FIRE AREA 59
137
EN-OP-104          Operability Determination Process Immediate Determination        4
04-1-01-E12-1
                  For Degraded of Nonconforming Conditions
Residual Heat Removal B Attachment IIIB
OTHER
137
    NUMBER                                     TITLE                               DATE
04-1-01-E12-1  
                  Russell Daniel Oil Co. Inc. Delivery Date Schedule          February 10,
Residual Heat Removal C Attachment IC
                                                                                  2011
137
CONDITION REPORT
04-1-01-E12-1
CR-GGN-2011-00198                CR-GGN-2011-00562              CR-GGN-2011-00654
Residual Heat Removal B Attachment VB
WORK ORDER
137
WO 52281566                      WO 52210679 03                 WO 52210679 02
04-1-01-E12-1
WO 52210679 01                  WO 00041743                    WO 52210679
Residual Heat Removal (Interface Valves) Attachment IIE
                                          A-5                                Attachment
137
04-1-01-P41-1
Standby Service Water System Attachment IIB
133
04-1-01-P41-1
Standby Service Water System Attachment IIIB
113
OTHER
NUMBER  
TITLE  
DATE  
11-4568
Scaffolding Evaluation Request
February 15,
2001
CALCULATION
NUMBER  
TITLE  
DATE  
9645
Diesel Generator Building Walls
August 2,  
1976
C-C400
SSW CT and Basin (Pump-House) Tornado and No
Earthquake
May 28, 1976
C-0-100
Diesel Generator Bldg. Walls Tornado Wind Load W
August 2,
1976
WORK ORDER  
WO 52256371
WO 00260559
WO 00259801
Section 1RO5:  Fire Protection
PROCEDURE
NUMBER
TITLE
REVISION
Fire Pre-Plan DG-03 Division II Diesel Generator Room
3
9A-343 - 9A347
GG UFSAR
Fire Pre-Plan A-02
RHR A Pump Room 1A103
1


ENGINEERING CHANGE
EC No. 24971                  EC No. 24904                  EC No. 24972
Section 1R07:
A-5
PROCEDURE
    NUMBER                                 TITLE                           REVISION
08-S-03-10      Chemistry Procedure-Closed Loops                                48
OTHER
    NUMBER                                  TITLE                              DATE
Attachment
CCE 2006-0002    Commitment Change Evaluation Form
PROCEDURE  
Letter          Response to Generic Letter 89-13; Service Water System      January 29,
NUMBER  
                Problems Affecting Safety-Related Equipment                    1990
TITLE  
WORK ORDER
REVISION  
WO 00178965 01                WO 00178965 02                WO 00178965 03
Fire Pre-Plan A-03  
Section 1R11: Licensed Operator Requalification Program
RCIC Pump Room 1A104
OTHER
1
    NUMBER                                 TITLE                           REVISION /
Fire Pre-Plan A-04
                                                                                DATE
RHR B Pump Room 1A105
GSMS-LOR-       LOR Training-Double Recirculation Pump Trip/ATWS            January 18,
1
WEX03                                                                          2011
9A.5.2.2
                                                                              Rev 17
Safe Shutdown Equipment
                Turnover and Simulator Differences 2011 Cycle 1 Simulator        1
                Training
Appendix 9B
                Per Control Room Walkdown, Modifications to TREX Load        January 7,
Fire Protection Program
                                                                                2011
Letter          Emergency Preparedness January 31, 2011 Simulator Drill    February 1,
                Performance Indicators                                        2011
CONDITION REPORT
                                        A-6                                Attachment
CR-GGN-2011-00862
CR-GGN-2011-01939
CR-GGN-2011-00851
CR-GGN-2011-00455
Section 1RO6: Flood Protection Measures
PROCEDURE
NUMBER  
TITLE  
REVISION /  
DATE  
9A-336 - 9A338
GG UFSAR
9A.5.59
GG UFSAR FIRE AREA 59
EN-OP-104
Operability Determination Process Immediate Determination
For Degraded of Nonconforming Conditions
4
OTHER
NUMBER
TITLE
DATE
Russell Daniel Oil Co. Inc. Delivery Date Schedule
February 10,  
2011  
CONDITION REPORT
CR-GGN-2011-00198
CR-GGN-2011-00562
CR-GGN-2011-00654
WORK ORDER
WO 52281566
WO 52210679 03
WO 52210679 02
WO 52210679 01
WO 00041743
WO 52210679


Section 1R12: Maintenance Effectiveness
PROCEDURE
    NUMBER                                   TITLE                         REVISION /
A-6
                                                                              DATE
EN-FP-S-001-   Engineering Standard-Appendix R Emergency Lighting Units    January 10,
Multi                                                                          2011
07-S-12-143    Big Beam Emergency Light Inspection, Battery Capacity            2
                Verification, and Functional Test
Attachment
EN-DC-203      Maintenance Rule Program                                        1
ENGINEERING CHANGE
EN-DC-206      Maintenance Rule (a)(1) Process                                  1
EN-DC-207      Maintenance Rule Periodic Assessment                            1
EC No. 24971
NMM EN-LI-118  Root Cause Evaluation Report Attachment IV (54 of 54)            12
EC No. 24904
EN-DC-205      Maintenance Rule Monitoring                                      2
EC No. 24972
                GG UFSAR Table 7.5-1 Safety-Related Display
                Instrumentation
Section 1R07:  
                GG UFSAR Table 7.5-2 Post-Accident Monitoring
                Instrumentation
PROCEDURE  
                GG UFSAR 6.3 Emergency Core Cooling Systems                      0
NUMBER  
03-1-01-3      Integrated Operating Instructions Plant Shutdown                118
TITLE  
OTHER
REVISION  
    NUMBER                                   TITLE                         REVISION /
08-S-03-10
                                                                              DATE
Chemistry Procedure-Closed Loops
                Emergency Lighting - GGNS Discussion of Recent Activities
48
                Maintenance Rule Expert Panel June 22, 2010 Meeting
                Minutes
OTHER
                Maintenance Rule Expert Panel August 10, 2010 Meeting
NUMBER
                Minutes
TITLE
                Entergy Nuclear-GGNS Maintenance Rule Program Basis              0
DATE
                Document, Control Room and Emergency Lighting (Z92)
CCE 2006-0002
                System
Commitment Change Evaluation Form
Z92            Maintenance Rule Database Control Room and Emergency
                Lighting
Letter
TM M348X.8001  Midtron 3200 Battery Conductance Tester
Response to Generic Letter 89-13; Service Water System
                                        A-7                              Attachment
Problems Affecting Safety-Related Equipment
January 29,
1990
WORK ORDER
WO 00178965 01
WO 00178965 02
WO 00178965 03  
Section 1R11:  Licensed Operator Requalification Program
OTHER  
NUMBER  
TITLE  
REVISION /  
DATE  
GSMS-LOR-
WEX03
LOR Training-Double Recirculation Pump Trip/ATWS
January 18,  
2011
Rev 17
Turnover and Simulator Differences 2011 Cycle 1 Simulator
Training
1
Per Control Room Walkdown, Modifications to TREX Load
January 7,
2011
Letter
Emergency Preparedness January 31, 2011 Simulator Drill
Performance Indicators
February 1,
2011


OTHER
  NUMBER                                 TITLE                             REVISION /
                                                                                DATE
A-7
VMA97/0181    Emergency Lights
              Maintenance Rule Database Information - Main Control          March 21,
              Room Air Conditioning (Z51) System                              2009 to
                                                                              December
                                                                              23, 2010
Attachment
              Maintenance Rule Database Z51 Control Room HVAC
Section 1R12:  Maintenance Effectiveness
              System
EC No.: 27856  Engineering Evaluation                                              0
PROCEDURE
              Maintenance Rule Program (a)(1) Evaluation and Action Plan
NUMBER  
              Main Control Room Air Conditioning (Z51) System
TITLE  
              Agenda for Maintenance Rule Expert Panel Meeting              February 4,
REVISION /  
                                                                                2010
DATE  
              RHR Heat Exchanger SSW Flow Indication (a)(1) Status
EN-FP-S-001-
              Maintenance Rule Database E12 RHR System
Multi
              Maintenance Rule Program (a)(1) Evaluation for the Residual
Engineering Standard-Appendix R Emergency Lighting Units
              Heat Removal (E12/RHR) System CR-GGN-2009-0754 CA
January 10,
              No. 002
2011
              Maintenance Rule (a)(1) Evaluation Standby Service Water
07-S-12-143
              (P41) System (GR-GGN-2010-00305)
Big Beam Emergency Light Inspection, Battery Capacity
              Agenda Items from Maintenance Rule Expert Panel Meeting        June 24,
Verification, and Functional Test
                                                                                2010
2
              Agenda Items from Maintenance Rule Expert Panel Meeting         June 22,
EN-DC-203
                                                                                2010
Maintenance Rule Program
CONDITION REPORT
1
CR-GGN -2009-05330          CR-GGN -2010-00381            CR-GGN -2010-04575
EN-DC-206
CR-GGN -2010-04585          CR-GGN -2010-06346            CR-GGN -2011-00481
Maintenance Rule (a)(1) Process
CR-GGN -2011-00521          CR-GGN -2011-01212            CR-GGN-2011-01650
1
CR-GGN-2010-01984          CR-GGN-2011-11505              CR-GGN-2011-01308
EN-DC-207
CR-GGN-2010-07315          CR-GGN-2009-00842              CR-GGN-2009-00754
Maintenance Rule Periodic Assessment
GR-GGN-2009-01729          CR-GGN-2009-02477              CR-GGN-2009-03394
1
CR-GGN-2009-02947          CR-GGN-2009-02848              CR-GGN-2009-03292
NMM EN-LI-118
CR-GGN-2009-03574          CR-GGN-2009-03592              CR-GGN-2009-04219
Root Cause Evaluation Report Attachment IV (54 of 54)  
                                      A-8                                  Attachment
12
EN-DC-205
Maintenance Rule Monitoring
2
GG UFSAR Table 7.5-1 Safety-Related Display
Instrumentation
GG UFSAR Table 7.5-2 Post-Accident Monitoring
Instrumentation
GG UFSAR 6.3 Emergency Core Cooling Systems
0
03-1-01-3
Integrated Operating Instructions Plant Shutdown
118
OTHER
NUMBER
TITLE
REVISION /
DATE
Emergency Lighting - GGNS Discussion of Recent Activities
Maintenance Rule Expert Panel June 22, 2010 Meeting
Minutes
Maintenance Rule Expert Panel August 10, 2010 Meeting  
Minutes
Entergy Nuclear-GGNS Maintenance Rule Program Basis
Document, Control Room and Emergency Lighting (Z92)
System
0
Z92
Maintenance Rule Database Control Room and Emergency
Lighting
TM M348X.8001
Midtron 3200 Battery Conductance Tester


CR-GGN-2010-01031            CR-GGN-2009-04048            CR-GGN-2009-05930
CR-GGN-2009-05215            CR-GGN-2009-05932            CR-GGN-2009-05472
CR-GGN-2009-06066            CR-GGN-2009-04733            CR-GGN-2010-00036
A-8
CR-GGN-2010-01329            CR-GGN-2011-00789            CR-GGN-2010-07351
CR-GGN-2010-04009            CR-GGN-2010-05892            CR-GGN-2011-00791
CR-GGN-2011-00820            CR-GGN-2011-00985            CR-GGN-2009-01204
CR-GGN-2010-00684            CR-GGN-2010-05290            CR-GGN-2010-01585
CR-GGN-2010-00800            CR-GGN-2010-01474            CR-GGN-2010-01337
Attachment
CR-GGN-2009-05508            CR-GGN-2010-01320            CR-GGN-2010-01345
OTHER
CR-GGN-2009-05731            CR-GGN-2009-06174            CR-GGN-2010-02797
NUMBER
CR-GGN-2010-02200            CR-GGN-2010-03655            CR-GGN-2010-04629
TITLE
CR-GGN-2010-02990            CR-GGN-2010-03241            CR-GGN-2009-00350
REVISION /
CR-GGN-2009-00426            CR-GGN-2009-00846            CR-GGN-2009-01518
DATE
CR-GGN-2010-02805            CR-GGN-2010-04015            CR-GGN-2010-03333
VMA97/0181
CR-GGN-2010-04625            CR-GGN-2010-04255            CR-GGN-2009-05527
Emergency Lights
CR-GGN-2010-02974            CR-GGN-2010-06137            CR-GGN-2010-05208
CR-GGN-2010-05330            CR-GGN-2010-04686            CR-GGN-2010-04963
CR-GGN-2010-05572            CR-GGN-2010-03650            CR-GGN-2010-06978
Maintenance Rule Database Information - Main Control
CR-GGN-2010-06148            CR-GGN-2010-06150            CR-GGN-2010-05328
Room Air Conditioning (Z51) System 
CR-GGN-2010-06142            CR-GGN-2011-00403            CR-GGN-2011-00749
March 21,
CR-GGN-2011-00819            CR-GGN-2011-00850            CR-GGN-2010-06895
2009 to
CR-GGN-2010-06918            CR-GGN-2011-01212            CR-GGN-2010-05147
December
WORK ORDER
23, 2010  
WO 52255810                  WO 52223396                  WO 52271013 01
WO 52196016                  WO 52220690
Maintenance Rule Database Z51 Control Room HVAC
Section 1R13: Maintenance Risk Assessment and Emergent Work Controls
System
PROCEDURE
  NUMBER                                TITLE                            REVISION
EC No.: 27856
EN-WM-101      On-line Work Management Process                                7
Engineering Evaluation
EN-WM-100      Work Request Generation, Screening and Classification          5
0
EN-WM-101      On-line Work Management Process                                8
EN-WM-101      On Line Emergent Work Addition/Deletion Approval Form for      7
Maintenance Rule Program (a)(1) Evaluation and Action Plan
                the Week of March 7, 2011
Main Control Room Air Conditioning (Z51) System
                                      A-9                                Attachment
Agenda for Maintenance Rule Expert Panel Meeting
February 4,
2010  
RHR Heat Exchanger SSW Flow Indication (a)(1) Status
Maintenance Rule Database E12 RHR System
Maintenance Rule Program (a)(1) Evaluation for the Residual
Heat Removal (E12/RHR) System CR-GGN-2009-0754 CA
No. 002
Maintenance Rule (a)(1) Evaluation Standby Service Water
(P41) System (GR-GGN-2010-00305)
Agenda Items from Maintenance Rule Expert Panel Meeting
June 24,
2010  
Agenda Items from Maintenance Rule Expert Panel Meeting
June 22,
2010  
CONDITION REPORT
CR-GGN -2009-05330
CR-GGN -2010-00381
CR-GGN -2010-04575
CR-GGN -2010-04585
CR-GGN -2010-06346
CR-GGN -2011-00481
CR-GGN -2011-00521
CR-GGN -2011-01212
CR-GGN-2011-01650
CR-GGN-2010-01984
CR-GGN-2011-11505
CR-GGN-2011-01308
CR-GGN-2010-07315
CR-GGN-2009-00842
CR-GGN-2009-00754
GR-GGN-2009-01729
CR-GGN-2009-02477
CR-GGN-2009-03394
CR-GGN-2009-02947
CR-GGN-2009-02848
CR-GGN-2009-03292
CR-GGN-2009-03574
CR-GGN-2009-03592
CR-GGN-2009-04219


PROCEDURE
  NUMBER                                TITLE                            REVISION
EN-WM-101      On Line Emergent Work Addition/Deletion Approval Form for      7
A-9
                the Week of February 28, 2011
WORK ORDER
WO250074                    WO247598                      WO52290243
WO52290462                  WO52290463                    WO52290464
WO70346                      WO52291451                    WO52291458
Attachment
WO52291454                  WO52291456                    WO52291689
CR-GGN-2010-01031
WO52291690                  WO261213                      WO52284287
CR-GGN-2009-04048
WO52269835                  WO52290236                    WO52290463
CR-GGN-2009-05930
WO52290464                  WO52291844                    WO52291454
CR-GGN-2009-05215
WO52291456                  WO261601                      WO250966-02
CR-GGN-2009-05932
WO237429                    WO256910-01                  WO52290639
CR-GGN-2009-05472
WO52287735                  WO52290638                    WO52287736
CR-GGN-2009-06066
WO52276935                  WO260417                      WO260212-02
CR-GGN-2009-04733
WO260212-01                  WO00219198                    WO260529-07
CR-GGN-2010-00036
WO52204865                  WO260503                      WO52243284
CR-GGN-2010-01329
WO260529-07                  WO52204865                    WO52199495
CR-GGN-2011-00789
WO255787-01,02,03,04        WO52249417                    WO52271012
CR-GGN-2010-07351
WO261175                    WO259639                      WO257881
CR-GGN-2010-04009
WO200935-02                  WO00257063                    WO224859
CR-GGN-2010-05892
WO261706                    WO255360-08                  WO263130
CR-GGN-2011-00791
WO261181-01 and 02          WO262143                      WO234988-04
CR-GGN-2011-00820
WO234992-04                  WO52250110-03                WO234985-04
CR-GGN-2011-00985
WO259003-05                  WO259005-05                  WO259007-05
CR-GGN-2009-01204
WO112951-08                  WO52270042                    WO52259286
CR-GGN-2010-00684
WO52275616                  WO52288663                    WO52290468
CR-GGN-2010-05290
WO52270252                  WO52291424                    WO52270250
CR-GGN-2010-01585
WO52291423                  WO235034                      WO52288844
CR-GGN-2010-00800
WO51563342                  WO160041                      WO52290473
CR-GGN-2010-01474
WO52281103
CR-GGN-2010-01337
                                    A-10                                Attachment
CR-GGN-2009-05508
CR-GGN-2010-01320
CR-GGN-2010-01345
CR-GGN-2009-05731
CR-GGN-2009-06174
CR-GGN-2010-02797
CR-GGN-2010-02200
CR-GGN-2010-03655
CR-GGN-2010-04629
CR-GGN-2010-02990
CR-GGN-2010-03241
CR-GGN-2009-00350
CR-GGN-2009-00426
CR-GGN-2009-00846
CR-GGN-2009-01518
CR-GGN-2010-02805
CR-GGN-2010-04015
CR-GGN-2010-03333
CR-GGN-2010-04625
CR-GGN-2010-04255
CR-GGN-2009-05527
CR-GGN-2010-02974
CR-GGN-2010-06137
CR-GGN-2010-05208
CR-GGN-2010-05330
CR-GGN-2010-04686
CR-GGN-2010-04963
CR-GGN-2010-05572
CR-GGN-2010-03650
CR-GGN-2010-06978
CR-GGN-2010-06148
CR-GGN-2010-06150
CR-GGN-2010-05328
CR-GGN-2010-06142
CR-GGN-2011-00403
CR-GGN-2011-00749
CR-GGN-2011-00819
CR-GGN-2011-00850
CR-GGN-2010-06895
CR-GGN-2010-06918
CR-GGN-2011-01212
CR-GGN-2010-05147
WORK ORDER
WO 52255810
WO 52223396
WO 52271013 01
WO 52196016
WO 52220690
Section 1R13:  Maintenance Risk Assessment and Emergent Work Controls
PROCEDURE
NUMBER
TITLE
REVISION
EN-WM-101
On-line Work Management Process
7
EN-WM-100
Work Request Generation, Screening and Classification
5
EN-WM-101
On-line Work Management Process
8
EN-WM-101
On Line Emergent Work Addition/Deletion Approval Form for
the Week of March 7, 2011
7


Section 1R15: Operability Evaluations
PROCEDURE
    NUMBER                                 TITLE                             REVISION
A-10
EN-OP-104      Operability Determination Process                                  4
EN-DC-115      EC No. 20228                                                      0
CALCULATION
    NUMBER                                  TITLE                            REVISION
PDS0170B        SSW Basin A Relief Valve                                        2
Attachment
DRAWING
PROCEDURE  
    NUMBER                                  TITLE                            REVISION
NUMBER  
FSK-M-KC187-    Design Change Drawing SSW Basin A and B                        8
TITLE  
01C1-Y
REVISION  
                Design Change Drawing Reinforced Concrete Distribution            8
EN-WM-101
                Support System Tower Elevation 157-8
On Line Emergent Work Addition/Deletion Approval Form for
OTHER
the Week of February 28, 2011
    NUMBER                                  TITLE                            REVISION /
7
                                                                                DATE
2007-029        LBDCR Initiation
WORK ORDER
                Grand Gulf Nuclear Station, Unity 1 - Conforming License    July 18, 2007
                Amendment to Incorporate the Mitigation Strategies Required
WO250074
                by Section B.5.b of the Commission Order EA - 02 - 026
WO247598
GNRO-           Supplementary Response Regarding Implementation Details      June 7, 2007
WO52290243
2007/00037      for the Phase 2 and 3 Mitigation Strategies Grand Gulf
WO52290462
                Nuclear Station
WO52290463
NEI 06-12      B.5.b Phase 2 & 3 Submittal Guideline                          Rev 2
WO52290464
                                                                              December
WO70346
                                                                                2006
WO52291451
7-15            GG FSAR                                                        Rev 59
WO52291458
9.5-3          GG UFSAR
WO52291454
Attachment 9.2  Immediate Determination for Degraded of Nonconforming
WO52291456
                Conditions CR-GGN-2011-01512
WO52291689
                                      A-11                                Attachment
WO52291690
WO261213
WO52284287
WO52269835
WO52290236
WO52290463
WO52290464
WO52291844
WO52291454
WO52291456
WO261601
WO250966-02
WO237429
WO256910-01
WO52290639
WO52287735
WO52290638
WO52287736
WO52276935
WO260417
WO260212-02
WO260212-01
WO00219198
WO260529-07
WO52204865
WO260503
WO52243284
WO260529-07
WO52204865
WO52199495
WO255787-01,02,03,04
WO52249417
WO52271012
WO261175
WO259639
WO257881
WO200935-02  
WO00257063
WO224859
WO261706
WO255360-08
WO263130
WO261181-01 and 02
WO262143
WO234988-04
WO234992-04
WO52250110-03
WO234985-04
WO259003-05
WO259005-05
WO259007-05
WO112951-08
WO52270042
WO52259286
WO52275616
WO52288663
WO52290468
WO52270252
WO52291424
WO52270250
WO52291423
WO235034
WO52288844
WO51563342
WO160041
WO52290473
WO52281103


OTHER
    NUMBER                                  TITLE                        REVISION /
                                                                            DATE
A-11
Attachment 9.5  Operability Evaluation CR-GGN-2011-00155
                NUS Switch Status
CONDITION REPORT
CR-GGN-2011-01173              CR-GGN-2011-00765            CR-GGN-2011-00155
CR-GGN-2011-00766              CR-GGN-2011-00799            CR-GGN-2011-01512
Attachment  
CR-GGN-2009-06838              CR-GGN-2011-01349            CR-GGN-2011-04701
CR-GGN-2011-00369              CR-GGN-2011-00643            CR-GGN-2011-00647
Section 1R15:  Operability Evaluations
CR-GGN-2011-00665              CR-GGN-2011-00666            CR-GGN-2011-00667
CR-GGN-2011-00668              CR-GGN-2011-00669            CR-GGN-2011-00670
PROCEDURE
CR-GGN-2011-00671
NUMBER
Section 1R18: Plant Modifications
TITLE
PROCEDURE
REVISION
    NUMBER                                 TITLE                         REVISION
EN-OP-104
EN-DC-136      Temporary Modifications                                        5
Operability Determination Process
EN-LI-102      Corrective Action Process                                    16
4
DRAWING
EN-DC-115
    NUMBER                                   TITLE                         REVISION
EC No. 20228
E-1187-007      E31 Leak Detection System RWCU Flow Circuit Computer          7
0
                Input
E1165014        Schematic Design Rod Control and Information System Rod      13
CALCULATION
                Position Information and SCRAM Time Test
NUMBER  
E1173028        Schematic Design Reactor Protection System Testability        6
TITLE  
M1051A          Main and Reheat System                                        33
REVISION  
OTHER
PDS0170B
    NUMBER                                   TITLE
SSW Basin A Relief Valve
                06-OP-1000-D-0001 Log Data
2
                                        A-12                             Attachment
DRAWING  
NUMBER  
TITLE  
REVISION  
FSK-M-KC187-
01C1-Y
Design Change Drawing SSW Basin A and B
8
Design Change Drawing Reinforced Concrete Distribution
Support System Tower Elevation 157-8
8
OTHER  
NUMBER  
TITLE  
REVISION /
DATE
2007-029
LBDCR Initiation
Grand Gulf Nuclear Station, Unity 1 - Conforming License
Amendment to Incorporate the Mitigation Strategies Required
by Section B.5.b of the Commission Order EA - 02 - 026
July 18, 2007
GNRO-
2007/00037
Supplementary Response Regarding Implementation Details
for the Phase 2 and 3 Mitigation Strategies Grand Gulf
Nuclear Station
June 7, 2007
NEI 06-12  
B.5.b Phase 2 & 3 Submittal Guideline
Rev 2
December
2006
7-15
GG FSAR
Rev 59
9.5-3
GG UFSAR
Attachment 9.2
Immediate Determination for Degraded of Nonconforming
Conditions CR-GGN-2011-01512


OTHER
    NUMBER                                 TITLE
CR-GGN-2009-   CR Periodic Review (initial at 6 months/follow by annual)
A-12
02198 CA 26    and/or Long Tem CA Classification Form
CONDITION REPORT
CR-GGN-2009-02198            CR-GGN-2010-04451                CR-GGN-2011-01231
WORK ORDER
WO00238932                    WO00238928                      WO00193921
Attachment
WO00193920                    WO002239736-01                  WO002239736-02
OTHER  
WO002239736-03
NUMBER  
ENGINEERING CHANGE
TITLE  
EC22768                      EC22625                          EC22635
REVISION /
Section 1R19: Postmaintenance Testing
DATE
PROCEDURE
Attachment 9.5
    NUMBER                                  TITLE                            REVISION /
Operability Evaluation CR-GGN-2011-00155
                                                                                DATE
06-OP-1E12-Q-   LPCI/RHR Subsystem A MOV Functional Test                        112
0005
NUS Switch Status
06-OP-1E12-Q-   LPCI/RHR Subsystem A Quarterly Functional Test                  121
0023
06-0P-1E12-     LPCI/RHR System B MOV Functional Test                            111
CONDITION REPORT  
0006
06-OP-1P41-Q-  Standby Service Water Loop A Valve AND Pump Operability          119
CR-GGN-2011-01173
0004            Test
CR-GGN-2011-00765
04-1-03-P75-1  Div 1 Diesel Generator Unexcited Run                              7
CR-GGN-2011-00155
06-OP-1P75-M-   Data Sheet III Standby Diesel Generator 11 Functional Test February 12,
CR-GGN-2011-00766
001                                                                            2011
CR-GGN-2011-00799
07-S-12-40      General Cleaning and Inspection of Rotating Electrical            2
CR-GGN-2011-01512
                Equipment
CR-GGN-2009-06838
07-S-12-146    General Maintenance Instruction Motor Off Line Diagnostic        1
CR-GGN-2011-01349
                                      A-13                                Attachment
CR-GGN-2011-04701
CR-GGN-2011-00369
CR-GGN-2011-00643
CR-GGN-2011-00647
CR-GGN-2011-00665
CR-GGN-2011-00666
CR-GGN-2011-00667
CR-GGN-2011-00668
CR-GGN-2011-00669
CR-GGN-2011-00670
CR-GGN-2011-00671
Section 1R18:  Plant Modifications
PROCEDURE
NUMBER
TITLE
REVISION
EN-DC-136
Temporary Modifications
5
EN-LI-102
Corrective Action Process
16
   
DRAWING
NUMBER
TITLE
REVISION
E-1187-007
E31 Leak Detection System RWCU Flow Circuit Computer
Input
7
E1165014
Schematic Design Rod Control and Information System Rod
Position Information and SCRAM Time Test
13
E1173028
Schematic Design Reactor Protection System Testability
6
M1051A
Main and Reheat System
33
OTHER
NUMBER
TITLE
06-OP-1000-D-0001 Log Data


PROCEDURE
    NUMBER                                 TITLE                           REVISION /
                                                                              DATE
A-13
              Data Acquisition
07-S-12-55    Insulation Resistance Testing                                    10
06-IC-1E22-QHPCS System Flow Rate - Low (Bypass) Functional Test            104
0004
OTHER
Attachment
    NUMBER                                TITLE                              DATE
OTHER
              RPS Motor GEN B - MCE Stator                                February 2,
NUMBER  
                                                                              2011
TITLE  
              HPCS Min Flow Valve Position                                March 18,
                                                                              2011
CR-GGN-2009-
DRAWING
02198 CA 26
    NUMBER                                 TITLE                             DATE
CR Periodic Review (initial at 6 months/follow by annual)
BRKR No. 52-   IC71SOOIOB
and/or Long Tem CA Classification Form
142229
BRKR No. 52-   IC7IS003B (Local C71-S003B)
142229
CONDITION REPORT
BRKR No. 52-   IC7IS003D (Local C71-S003D)
142229
CR-GGN-2009-02198
              Timeline for Events leading to NRC Notification Call on      March 18,
CR-GGN-2010-04451
              HPCS                                                          2011
CR-GGN-2011-01231
CONDITION REPORT
CR-GGN-2011-00945
WORK ORDER
WORK ORDER
   
WO52311451                  WO52311569                      WO52285575
WO00238932
WO00251847                  WO52224645                      WO52223715
WO00238928
WO00262318                  WO00259110-01                  WO00259110-03
WO00193921
WO00237650-01                WO00237650-04                  WO00237650-05
WO00193920
WO00237650-06                WO52304041                      WO00270205-01
WO002239736-01
                                      A-14                              Attachment
WO002239736-02
WO002239736-03
ENGINEERING CHANGE
EC22768
EC22625
EC22635
Section 1R19:  Postmaintenance Testing
PROCEDURE
NUMBER  
TITLE  
REVISION /
DATE  
06-OP-1E12-Q-
0005
LPCI/RHR Subsystem A MOV Functional Test
112
06-OP-1E12-Q-
0023
LPCI/RHR Subsystem A Quarterly Functional Test
121
06-0P-1E12-
0006
LPCI/RHR System B MOV Functional Test
111
06-OP-1P41-Q-
0004
Standby Service Water Loop A Valve AND Pump Operability
Test
119
04-1-03-P75-1
Div 1 Diesel Generator Unexcited Run
7
06-OP-1P75-M-
001
Data Sheet III Standby Diesel Generator 11 Functional Test
February 12,
2011
07-S-12-40
General Cleaning and Inspection of Rotating Electrical
Equipment 
2
07-S-12-146
General Maintenance Instruction Motor Off Line Diagnostic
1


WO00270205-02
Section 1R22: Surveillance Testing
PROCEDURE
A-14
    NUMBER                                 TITLE                             REVISION
06-CH-1B21-O-  Reactor Coolant Routine Chemistry-Sample February 23,            106
0002            2011
06-CH-1B21-O-   Reactor Coolant Routine Chemistry-Sample February 18,             106
0002            2011
Attachment
06-CH-1B21-O-  Plant Operations Manual-Reactor Coolant Routine Chemistry        106
PROCEDURE  
0002
NUMBER  
06-CH-1B21-W-  Reactor Coolant Dose Equivalent Iodine                            104
TITLE  
0008
REVISION /
06-OP-1C61-R-  Functional Checks with E51 Valves                                109
DATE
0002
Data Acquisition
06-OP-1P75-M-   Standby Diesel Generator Functional Test                          132
07-S-12-55
0001
Insulation Resistance Testing
06-IC-1D17-R-  Fuel Handling Area Ventilation Exhaust High High Radiation        102
10
0010            Electronics Time Response Test
06-IC-1E22-Q-
04-1-01-P81-1  High Pressure Core Spray Diesel Generator                          67
0004
06-OP-1P81-M-  HPCS Diesel Generator 13 Functional Test                          123
HPCS System Flow Rate - Low (Bypass) Functional Test
0002
104
EN-OP-109      Conduct of Operations                                              2
OTHER
OTHER
    NUMBER                                  TITLE                                DATE
NUMBER
                Drywell Unidentified Leakage Rate vs. A Recirc Seal Delta  June 2010-
TITLE
                T                                                            January 2011
DATE
CONDITION REPORT
CR-GGN-2011-01932            CR-GGN-2011-01868
RPS Motor GEN B - MCE Stator
WORK ORDER
February 2,
WO52271012                    WO52289870                    WO52288401
2011
WO52261837                    WO52307262                    WO00270146-01
                                      A-15                                Attachment
HPCS Min Flow Valve Position 
March 18,  
2011  
DRAWING
NUMBER
TITLE
DATE
BRKR No. 52-
142229
IC71SOOIOB
BRKR No. 52-
142229
IC7IS003B (Local C71-S003B)
BRKR No. 52-
142229
IC7IS003D (Local C71-S003D)
Timeline for Events leading to NRC Notification Call on
HPCS
March 18,
2011  
CONDITION REPORT  
CR-GGN-2011-00945
WORK ORDER
WO52311451
WO52311569
WO52285575
WO00251847
WO52224645
WO52223715
WO00262318
WO00259110-01
WO00259110-03
WO00237650-01
WO00237650-04
WO00237650-05
WO00237650-06
WO52304041
WO00270205-01


Section 1EP6: Drill Evaluation
OTHER
      NUMBER                       TITLE                       DATE
A-15
                    Emergency Facility Log                      March 3, 2011
                    Repair and Corrective Action Table          March 3, 2011
Emergency Notification Form 1-7 for EP Drill                    March 3, 2011
GGNS 2011 1st Quarter ERO Training Drill
CONDITION REPORT
Attachment
CR-GGN-2011-01481              CR-GGN-2011-01486                CR-GGN-2011-01495
WO00270205-02
CR-GGN-2011-01499              CR-GGN-2011-01510                CR-GGN-2011-01519
CR-GGN-2011-01520              CR-GGN-2011-01522
Section 2RS01: Radiological Hazard Assessment and Exposure Controls
PROCEDURES
Section 1R22: Surveillance Testing
    NUMBER                                    TITLE                              REVISION
EN-RP-100        Radiation Worker Expectations                                      6
PROCEDURE
EN-RP-101        Access Control for Radiologically Controlled Areas                  5
NUMBER  
EN-RP-102       Radiological Control                                                2
TITLE  
EN-RP-106        Radiological Survey Documentation                                  2
REVISION
01-S-08-1       Administration of the GGNS Radiation Protection Program            105
06-CH-1B21-O-
01-S-08-6        Radioactive Source Control                                        113
0002
08-S-02-50      Radiological Surveys and Surveillances                            116
Reactor Coolant Routine Chemistry-Sample February 23,  
AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES
2011
    NUMBER                               TITLE                               DATE
106
LO-GLO-2010-93    Pre-NRC Rad Hazard Assessment and Exposure            December 16, 2010
                  Controls Assessment
06-CH-1B21-O-
CONDITION REPORTS
0002
CR-GGN-2011-00183 CR-GGN-2011-00551 CR-GGN-2011-00655 CR-GGN-2011-00926
Reactor Coolant Routine Chemistry-Sample February 18,
CR-GGN-2011-00740
2011
                                        A-16                                  Attachment
106
06-CH-1B21-O-
0002
Plant Operations Manual-Reactor Coolant Routine Chemistry
106
06-CH-1B21-W-
0008
Reactor Coolant Dose Equivalent Iodine
104
06-OP-1C61-R-
0002
Functional Checks with E51 Valves
109
06-OP-1P75-M-
0001
Standby Diesel Generator Functional Test
132
06-IC-1D17-R-
0010
Fuel Handling Area Ventilation Exhaust High High Radiation  
Electronics Time Response Test
102  
04-1-01-P81-1  
High Pressure Core Spray Diesel Generator
67
06-OP-1P81-M-
0002
HPCS Diesel Generator 13 Functional Test
123
EN-OP-109
Conduct of Operations 
2
OTHER
NUMBER  
TITLE  
DATE  
Drywell Unidentified Leakage Rate vs. A Recirc Seal Delta
T
June 2010-  
January 2011
CONDITION REPORT
CR-GGN-2011-01932
CR-GGN-2011-01868
WORK ORDER
WO52271012
WO52289870
WO52288401
WO52261837
WO52307262
WO00270146-01


RADIOLOGICAL SURVEY
    NUMBER                               TITLE                                 DATE
GG-1102-0146    Routine Daily Surveys                                  February 15, 2011
A-16
GG-1012-0083    208 CTMT Entire Elevation                              December 7, 2010
GG-1102-0152    208 CTMT Entire Elevation                              February 15, 2011
GG-1012-0118    119 AB RHR A Room                                      December 9, 2010
GG-1012-0086    119 AB RHR A Room                                      February 7, 2011
GG-1011-0254    119 AB RHR B Room                                      November 30, 2010
Attachment
GG-1101-0156    119 AB RHR B Room                                      January 16, 2011
GG-1011-0064    93 Aux RHR C & ADHR Hx Rooms                            November 6, 2010
Section 1EP6:  Drill Evaluation
GG-1102-0044    93 Aux RHR C & ADHR Hx Rooms                            February 3, 2011
GG-1011-0018    119 Aux Piping Penetration & Valve Room                November 2, 2010
OTHER
GG-1102-0041    119 Aux Piping Penetration & Valve Room                February 3, 2011
GG-1011-0063    93 Aux HPCS Pump Room                                  November 6, 2010
GG-1102-0042    93 Aux HPCS Pump Room                                  February 3, 2011
NUMBER  
RADIATION WORK PERMITS
    NUMBER                                    TITLE
20101005        Tours and Inspections into all areas
TITLE
20111054        Locked High Radiation Area Entries for Plant/System Investigations, Valve
                Manipulations, Tagouts, and Misc. Activities
20111058        Maintenance in HRA /HCA & Above
DATE  
Section 2RS02: Occupational ALARA Planning and Controls
PROCEDURES
    NUMBER                                 TITLE                             REVISION
EN-RP-105      Radiological Work Permits                                          9
EN-RP-110      ALARA Program                                                       7
Emergency Facility Log
AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES
    NUMBER                               TITLE                                 DATE
LO # LO-GLO-   Pre-NRC Inspection for ALARA Planning and Controls-    November 9, 2010
March 3, 2011
2010-00094      Assessment
CONDITION REPORTS
                                      A-17                                  Attachment
Repair and Corrective Action Table 
March 3, 2011  
Emergency Notification Form 1-7 for EP Drill
March 3, 2011
GGNS 2011 1st  Quarter ERO Training Drill
CONDITION REPORT
CR-GGN-2011-01481
CR-GGN-2011-01486
CR-GGN-2011-01495
CR-GGN-2011-01499
CR-GGN-2011-01510
CR-GGN-2011-01519
CR-GGN-2011-01520
CR-GGN-2011-01522
Section 2RS01: Radiological Hazard Assessment and Exposure Controls
PROCEDURES  
NUMBER  
TITLE  
REVISION  
EN-RP-100
Radiation Worker Expectations
6
EN-RP-101
Access Control for Radiologically Controlled Areas
5
EN-RP-102
Radiological Control
2
EN-RP-106
Radiological Survey Documentation
2
01-S-08-1
Administration of the GGNS Radiation Protection Program  
105
01-S-08-6
Radioactive Source Control
113
08-S-02-50
Radiological Surveys and Surveillances
116
AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES  
NUMBER  
TITLE  
DATE  
LO-GLO-2010-93
Pre-NRC Rad Hazard Assessment and Exposure
Controls Assessment
December 16, 2010  
CONDITION REPORTS  
CR-GGN-2011-00183 CR-GGN-2011-00551 CR-GGN-2011-00655 CR-GGN-2011-00926
CR-GGN-2011-00740 


CR-GGN-2011-00425 CR-GGN-2011-00425 CR-GGN-2010-06335
RADIATION WORK PERMIT PACKAGES
    NUMBER                                  TITLE
A-17
2010-1402      Refuel Floor High Water Activities
2010-1403      Reactor Disassemble/Reassemble
2010-1508      Under Vessel Activities
2010-1530      B Recirc Pump Replacement
2010-1534      B21F011B Stem Replacement
Attachment
Section 4OA1: Performance Indicator Verification
RADIOLOGICAL SURVEY 
PROCEDURE
  NUMBER                                  TITLE                      REVISION
NUMBER
                st
TITLE
EN-LI-114      1 Quarter 2010 Unplanned Scrams per 7,000 Critical        4
DATE
                Hours
EN-LI-114      2nd Quarter 2010 Unplanned Scrams per 7,000 Critical      4
GG-1102-0146
                Hours
Routine Daily Surveys
EN-LI-114      3rd Quarter 2010 Unplanned Scrams per 7,000 Critical      4
February 15, 2011  
                Hours
GG-1012-0083
EN-LI-114      4th Quarter 2010 Unplanned Scrams per 7,000 Critical      4
208 CTMT Entire Elevation
                Hours
December 7, 2010
EN-LI-114      1st Quarter 2010 Unplanned Scrams with Complications      4
GG-1102-0152
EN-LI-114      2nd Quarter 2010 Unplanned Scrams with Complications      4
208 CTMT Entire Elevation
EN-LI-114      3rd Quarter 2010 Unplanned Scrams with Complications      4
February 15, 2011
EN-LI-114      4th Quarter 2010 Unplanned Scrams with Complications      4
GG-1012-0118
EN-LI-114      1st Quarter 2010 Unplanned Power Changes per 7,000        4
119 AB RHR A Room
                Critical Hours
December 9, 2010  
EN-LI-114      2nd Quarter 2010 Unplanned Power Changes per 7,000        4
GG-1012-0086
                Critical Hours
119 AB RHR A Room
EN-LI-114      3rd Quarter 2010 Unplanned Power Changes per 7,000        4
February 7, 2011
                Critical Hours
GG-1011-0254
EN-LI-114      4th Quarter 2010 Unplanned Power Changes per 7,000        4
119 AB RHR B Room
                Critical Hours
November 30, 2010  
                                        A-18                        Attachment
GG-1101-0156
119 AB RHR B Room
January 16, 2011
GG-1011-0064
93 Aux RHR C & ADHR Hx Rooms
November 6, 2010
GG-1102-0044
93 Aux RHR C & ADHR Hx Rooms
February 3, 2011
GG-1011-0018
119 Aux Piping Penetration & Valve Room
November 2, 2010  
GG-1102-0041
119 Aux Piping Penetration & Valve Room
February 3, 2011
GG-1011-0063
93 Aux HPCS Pump Room
November 6, 2010  
GG-1102-0042
93 Aux HPCS Pump Room
February 3, 2011
RADIATION WORK PERMITS
NUMBER
TITLE
20101005
Tours and Inspections into all areas 
20111054
Locked High Radiation Area Entries for Plant/System Investigations, Valve
Manipulations, Tagouts, and Misc. Activities
20111058
Maintenance in HRA /HCA & Above
Section 2RS02:  Occupational ALARA Planning and Controls
PROCEDURES
NUMBER
TITLE
REVISION
EN-RP-105
Radiological Work Permits
9
EN-RP-110
ALARA Program
7  
AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES
NUMBER
TITLE
DATE
LO # LO-GLO-
2010-00094
Pre-NRC Inspection for ALARA Planning and Controls-
Assessment
November 9, 2010  
CONDITION REPORTS


OTHER
  NUMBER                                   TITLE
                January 2010 Core Thermal Power
A-18
                February 2010 Core Thermal Power
                March 2010 Core Thermal Power
                April 2010 Core Thermal Power
                May 2010 Core Thermal Power
                June 2010 Core Thermal Power
Attachment
                July 2010 Core Thermal Power
CR-GGN-2011-00425 CR-GGN-2011-00425  CR-GGN-2010-06335
                August 2010 Core Thermal Power
                September 2010 Core Thermal Power
                October 2010 Core Thermal Power
RADIATION WORK PERMIT PACKAGES
                November 2010 Core Thermal Power
                December 2010 Core Thermal Power
NUMBER  
Section 4OA2: Identification and Resolution of Problems
TITLE  
OTHER
  NUMBER                                  TITLE                          DATE
                GGNS Position on Riley Temperature Switch Replacement
2010-1402
                Maintenance Rule Program Functional Failures-Riley
Refuel Floor High Water Activities
                Temperature Switches
                NUS Switch Status                                      February 2,
2010-1403
                                                                          2011
Reactor Disassemble/Reassemble
                Riley History Discussion by Lee Eaton
                Riley History Presentation to 2009 PInR
2010-1508
CONDITION REPORT
Under Vessel Activities
CR-GGN-2009-05879
                                      A-19                          Attachment
2010-1530
B Recirc Pump Replacement
2010-1534
B21F011B Stem Replacement
Section 4OA1:  Performance Indicator Verification
PROCEDURE
NUMBER
TITLE
REVISION
EN-LI-114
1st Quarter 2010 Unplanned Scrams per 7,000 Critical
Hours
4
EN-LI-114
2nd Quarter 2010 Unplanned Scrams per 7,000 Critical
Hours
4
EN-LI-114
3rd  Quarter 2010 Unplanned Scrams per 7,000 Critical
Hours
4
EN-LI-114
4th Quarter 2010 Unplanned Scrams per 7,000 Critical
Hours
4
EN-LI-114
1st Quarter 2010 Unplanned Scrams with Complications
4
EN-LI-114
2nd  Quarter 2010 Unplanned Scrams with Complications
4
EN-LI-114
3rd Quarter 2010 Unplanned Scrams with Complications
4
EN-LI-114
4th Quarter 2010 Unplanned Scrams with Complications
4
EN-LI-114
1st Quarter 2010 Unplanned Power Changes per 7,000
Critical Hours
4
EN-LI-114
2nd Quarter 2010 Unplanned Power Changes per 7,000
Critical Hours
4
EN-LI-114
3rd Quarter 2010 Unplanned Power Changes per 7,000
Critical Hours
4
EN-LI-114
4th Quarter 2010 Unplanned Power Changes per 7,000
Critical Hours
4


Section 4OA3: Event Follow-Up
PROCEDURE
  NUMBER                                   TITLE                           REVISION
A-19
EN-DC-167      Classification of Structures, Systems, and Components              3
EN-HU-103      Human Performance Error Reviews for CR-GGN-2010-7877              4
EN-DC-115      Engineering Change Process                                        11
DRAWINGS
  NUMBER                                    TITLE                          REVISION
Attachment
M-1127A        Piping and Instrumentation Diagram Noblechem Monitoring            0
OTHER
                System
NUMBER  
M-1081B        Control Rod Drive Hydraulic System                                28
TITLE  
M-1078A        Reactor Recirculation System Unit 1                              33
M-1079          Reactor Water Clean-up System Unit 1                              46
M-1069A        Process Sampling System Unit 1                                    24
January 2010 Core Thermal Power
OTHER
  NUMBER                                    TITLE                              DATE
                Root Cause Evaluation Report-Control Room Air Conditioner    October 16,
February 2010 Core Thermal Power
                B Trip (Event Date 10-14-2010)                                  2010
GNRO-          LER 2010-002-00Control Room Air Conditioning                  December
2010/00077                                                                    13, 2010
March 2010 Core Thermal Power
                Root Cause Evaluation Report Mitigation Monitor Durability November 8,
                Monitor Pump Failure                                            2010
                MMS Skid Piping/Component Design Basis
April 2010 Core Thermal Power
                Compliance with NRC Regulatory Guide 1.26
CONDITION REPORT
CR-GGN-2010-07315              CR-GGN-2010-08580              CR-GGN-2010-07852
May 2010 Core Thermal Power
ENGINEERING CHANGE
                                        A-20                              Attachment
June 2010 Core Thermal Power
July 2010 Core Thermal Power
August 2010 Core Thermal Power
September 2010 Core Thermal Power
October 2010 Core Thermal Power
   
November 2010 Core Thermal Power
December 2010 Core Thermal Power
Section 4OA2:  Identification and Resolution of Problems
OTHER
NUMBER
TITLE
DATE
GGNS Position on Riley Temperature Switch Replacement
Maintenance Rule Program Functional Failures-Riley
Temperature Switches
NUS Switch Status
February 2,  
2011
Riley History Discussion by Lee Eaton
Riley History Presentation to 2009 PInR
CONDITION REPORT  
CR-GGN-2009-05879


EC13135                       EC13132                         EC13138
Section 4OA5 Temporary Instruction 2515/179
PROCEDURES
A-20
    NUMBER                                   TITLE                       REVISION
EN-RP-143         Source Control                                             7
MISCELLANEOUS DOCUMENTS
      TITLE                                                               DATE
National Source Tracking System Annual Inventory Reconciliation Report     2010
Attachment
National Source Tracking System Annual Inventory Reconciliation Report     2011
Section 4OA7: Licensee-Identified Violations
CONDITION REPORT
Section 4OA3:  Event Follow-Up
PROCEDURE
NUMBER
TITLE
REVISION
EN-DC-167
Classification of Structures, Systems, and Components
3
EN-HU-103
Human Performance Error Reviews for CR-GGN-2010-7877
4
EN-DC-115
Engineering Change Process
11
DRAWINGS
NUMBER
TITLE
REVISION
M-1127A
Piping and Instrumentation Diagram Noblechem Monitoring
System
0
M-1081B
Control Rod Drive Hydraulic System
28
M-1078A
Reactor Recirculation System Unit 1
33
M-1079
Reactor Water Clean-up System Unit 1
46
M-1069A
Process Sampling System Unit 1
24
OTHER
NUMBER
TITLE
DATE
Root Cause Evaluation Report-Control Room Air Conditioner
B Trip (Event Date 10-14-2010)
October 16,
2010
GNRO-
2010/00077
LER 2010-002-00Control Room Air Conditioning
December
13, 2010
Root Cause Evaluation Report Mitigation Monitor Durability
Monitor Pump Failure 
November 8,
2010
MMS Skid Piping/Component Design Basis
Compliance with NRC Regulatory Guide 1.26
CONDITION REPORT
CR-GGN-2010-07315
CR-GGN-2010-08580
CR-GGN-2010-07852
ENGINEERING CHANGE
 
A-21
Attachment
EC13135  
EC13132  
EC13138  
Section 4OA5 Temporary Instruction 2515/179  
PROCEDURES  
NUMBER  
TITLE  
REVISION  
EN-RP-143  
Source Control  
7  
MISCELLANEOUS DOCUMENTS  
TITLE  
DATE  
National Source Tracking System Annual Inventory Reconciliation Report  
2010  
National Source Tracking System Annual Inventory Reconciliation Report  
2011  
Section 4OA7: Licensee-Identified Violations  
CONDITION REPORT
CR-GGN-2011-00851
CR-GGN-2011-00851
                                        A-21                          Attachment
}}
}}

Latest revision as of 06:25, 13 January 2025

IR 05000416-11-002; on 01/21/2011 – 03/27/2011; Grand Gulf Nuclear Station, Integrated Resident and Regional Report; Fire Protection, Maintenance Effectiveness, Radiological Hazard Assessment and Exposure Controls, and Event Follow-Up
ML111300462
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 05/10/2011
From: Vincent Gaddy
NRC/RGN-IV/DRP/RPB-C
To: Mike Perito
Entergy Operations
References
IR-11-002
Download: ML111300462 (61)


See also: IR 05000416/2011002

Text

May 10, 2011

Mr. Mike Perito

Vice President Operations

Entergy Operations, Inc.

Grand Gulf Nuclear Station

P.O. Box 756

Port Gibson, MS 39150

Subject: GRAND GULF NRC INTEGRATED INSPECTION REPORT NUMBER

05000416/2011002

Dear Mr. Perito:

On March 27, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at your Grand Gulf Nuclear Station. The enclosed integrated inspection report documents the

inspection findings, which were discussed on April 14, 2011, with Mike Perito, Vice President

Operations, and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the NRC has determined that one Severity Level IV

violation of NRC requirements occurred. The NRC has also identified five issues that were

evaluated under the risk significance determination process as having very low safety

significance (Green). The NRC has determined that four of these findings have violations

associated with these issues. Additionally, one licensee-identified violation, which was

determined to be of very low safety significance, is listed in this report. However, because of

their very low safety significance and because they were entered into your corrective action

program, the NRC is treating these findings as noncited violations, consistent with Section 2.3.2

of the NRC Enforcement Policy.

If you contest the significance of the noncited violations, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with

copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV,

612 E. Lamar Blvd, Suite 400, Arlington, Texas, 76011-4125; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the

NRC Resident Inspector at the facility. In addition, if you disagree with the cross-cutting aspect

assigned to any finding in this report, you should provide a response within 30 days of the date

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

Entergy Operations, Inc.

- 2 -

of this inspection report, with the basis for your disagreement, to the Regional Administrator,

Region IV, and the NRC Resident Inspector at the facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosures, and your response, if you choose to provide one, will be made available

electronically for public inspection in the NRC Public Document Room or from the NRC's

document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html. To the extent possible, your response should not include any personal privacy

or proprietary, information so that it can be made available to the Public without redaction.

Sincerely,

/RA/

Vincent Gaddy, Chief

Project Branch C

Division of Reactor Projects

Docket: 50-416

License: NPF-29

Enclosed: NRC Inspection Report 05000416/2011002

w/Attachment: Supplemental Information

Distribution via ListServe

Entergy Operations, Inc.

- 3 -

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Art.Howell@nrc.gov)

DRP Director (Kriss.Kennedy@nrc.gov)

DRP Deputy Director (Troy.Pruett@nrc.gov)

DRS Director (Anton.Vegel@nrc.gov)

Senior Resident Inspector (Rich.Smith@nrc.gov)

Branch Chief, DRP/C (Vincent.Gaddy@nrc.gov)

Senior Project Engineer, DRP/C (Bob.Hagar@nrc.gov)

Project Engineer, DRP/C (Rayomand.Kumana@nrc.gov)

GG Administrative Assistant (Alley.Farrell@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Alan.Wang@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

RIV OEDO/ETA (Stephanie Bush-Goddard@nrc.gov)

OEMail Resource

ROP Reports

File located: R:\\_REACTORS\\_GG\\GG 2011002 RP-RLS-vgg.docx

SUNSI Rev Compl.

Yes No

ADAMS

Yes No

Reviewer Initials

VGG

Publicly Avail

Yes No

Sensitive

Yes No

Sens. Type Initials

VGG

SRI:DRP/PBC

SPE:DRP/PBC

C:DRS/EB1

C:DRS/EB2

RLSmith

BHagar

TRFarnholtz

NFOKeefe

/RA/RCHagar for

/RA/

/RA/

/RA/

5/4/2011

5/4/2011

4/21/2011

4/15/2011

C:DRS/OB

C:TSS

C:DRS/PSB1

C:DRS/PSB2

C:ACES/SAC

MHaire

MHay

MPShannon

GEWerner

NTaylor

/RA/

/RA/

/RA/

/RA/

/RA/

4/15/2011

4/18/2011

4/18/2011

4/15/2011

4/18/2011

C:DRP/C

VGaddy

/RA/

5/10/11

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

- 1 -

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

05000416

License:

NPF-29

Report:

05000416/2011002

Licensee:

Entergy Operations, Inc.

Facility:

Grand Gulf Nuclear Station

Location:

7003 Baldhill Road

Port Gibson, MS 39150

Dates:

January 21, 2011, through March 27, 2011

Inspectors:

R. Smith, Senior Resident Inspector

M. Baquera, Resident Inspector, Palo Verde

A. Fairbanks, Reactor Inspector

C. Graves, Health Physicist

L. Ricketson, P.E., Senior Health Physicist

E. Uribe, Reactor Inspector

Approved By:

Vincent Gaddy, Chief, Project Branch C

Division of Reactor Projects

- 2 -

Enclosure

SUMMARY OF FINDINGS

IR 05000416/2011002; 1/1/2011 - 3/27/2011; Grand Gulf Nuclear Station, Integrated Resident

and Regional Report; Fire Protection, Maintenance Effectiveness, Radiological Hazard

Assessment and Exposure Controls, and Event Follow-Up.

The report covered a 3-month period of inspection by resident inspectors and an announced

baseline inspection by region-based inspectors. Five Green noncited violations of significance

were identified and one Green finding of significance was identified. The significance of most

findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual

Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined

using Inspection Manual Chapter 0310, Components Within the Cross Cutting Areas. Findings

for which the significance determination process does not apply may be Green or be assigned a

severity level after NRC management review. The NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 4, dated December 2006.

A.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Mitigating Systems

SLIV. Inspectors identified a noncited violation of 10 CFR 50.71(e)(4), which

requires the final safety analysis report be updated, at intervals not exceeding 24

months, to reflect changes made in the facility or procedures described in the

final safety analysis report. Licensee personnel failed to update the original

revision of the final safety analysis report to reflect the actual number of low

pressure coolant injection loops available for automatic initiation during shutdown

cooling operations in Mode 3. The licensee plans to update the final safety

analysis report at the next scheduled revision. This finding was entered into the

licensees corrective action program as condition report CR-GGN-2011-01631.

The failure of licensing personnel to update the final safety analysis report to

reflect the available low pressure coolant injection loops for automatic initiation

during shutdown cooling operations in Mode 3 was a performance deficiency.

This finding was evaluated using traditional enforcement because it had the

potential for impacting the NRCs ability to perform its regulatory function. The

inspectors used the NRC Enforcement Policy, dated September 30, 2010, to

evaluate the significance of this violation. Consistent with the NRC Enforcement

Policy, this finding was determined to be a Severity Level IV noncited violation.

Green. The inspectors identified a noncited violation of 10 CFR Part 50.65(a)(2)

for the licensees failure to demonstrate that the performance of the train B

control room air conditioner was being effectively controlled through the

performance of appropriate preventive maintenance. Engineering did not

properly evaluate maintenance rule functional failures resulting in the system

remaining in an a(2) status instead of an a(1) status. As corrective action, the

- 3 -

Enclosure

train B control room air conditioner was moved into an a(1) status. The licensee

entered this issue into their corrective action program as Condition Report

CR-GGN-2011-01623.

The finding was more than minor because it was associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and adversely

affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Inspectors performed a Phase 1 screening, in accordance with

Inspection Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and

Characterization of Findings, and determined that the finding was of very low

safety significance (Green) because the maintenance rule aspect of the finding

did not cause an actual loss of safety function of the system nor did it cause a

component to be inoperable. As corrective action, the train B control room air

conditioner was moved into an (a)(1) status. This finding had a crosscutting

aspect in the area of human performance associated with the decision making

component because licensee personnel failed to make appropriate safety-

significant or risk-significant decisions to address the multiple failures of the train

B control room air conditioner compressor. H.1(a) (Section 1R12.b.2)

Green. The inspectors reviewed a self-revealing noncited violation of 10 CFR

Part 50, Appendix B, Criterion XVI, Corrective Action, after the licensee failed to

determine the cause and prevent recurrence of a significant condition adverse to

quality associated with the train B control room air conditioner compressor

tripping due to low oil pressure. Specifically, on December 13, 2010, the train B

control room air conditioner compressor tripped on low oil pressure after the

licensee had performed a root cause analysis to identify the cause and prevent

recurrence of a similar compressor trip on October 14, 2010. As immediate

corrective action, the licensee installed an inline suction filter. No additional

failures have occurred since its installation. The finding was entered into the

licensees corrective action program as Condition Report CR-GGN-2010-07315.

This finding was more than minor because it was associated with the equipment

performance attribute of the Mitigating Systems Cornerstone and adversely

affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 worksheets, the inspectors determined that a

Phase 2 analysis was required because the finding represented a loss of system

safety function. The plant-specific risk informed notebook does not include the

evaluation of risk caused by the loss of cooling to the main control room.

Therefore, the senior reactor analyst conducted a Phase 3 analysis. Based on

the bounding analysis, the analyst determined that the change in core damage

frequency result was 5.9 x 10-7. This noncited violation was therefore determined

to be of very low safety significance (Green). This finding had a crosscutting

aspect in the area of problem identification and resolution associated with the

corrective action program component because licensee personnel failed to

- 4 -

Enclosure

thoroughly evaluate the multiple failures of the train B control room air conditioner

compressor. P.1(c) (Section 4OA3.1.b)

Cornerstone: Barrier Integrity

Green

. The inspectors identified a noncited violation of Facility Operating License

Condition 2.C(41), involving the failure to ensure that transient combustible were

not stored in the fire exclusion zone near the independent spent fuel storage

installation. The inspectors performed a quarterly fire protection inspection of

independent spent fuel storage installation and identified a large air conditioner

with combustible material covering it located in the fire exclusion zone that was

within 60 feet of the dry fuel storage pad. The inspectors determined through

interviews that the material had been placed there the previous day by the

maintenance department. As immediate corrective action the licensee removed

the combustible material from the area. The finding was entered into the

licensees corrective action program as Condition Report CR-GGN-2011-00455.

This finding was more than minor because it was associated human performance

attribute of the Barrier Integrity Cornerstone to provide reasonable assurance

that physical design barriers protect the public from radionuclide releases caused

by accidents or events. Using Manual Chapter 0609, Appendix F, Fire

Protection Significance Determination Process, the inspectors determined that

the finding impacted the fire prevention and administrative controls category.

The inspectors assigned a low degradation rating due to the fact that the amount

of combustible material in the area was minimal. The inspectors concluded that

the finding was of very low safety significance (Green) due to the fact there were

no fire ignition sources in the area. The cause of this finding has a crosscutting

aspect in the area of human performance associated with the work practices

component because the licensee failed to effectively communicate expectations

regarding storage of combustible material near the dry fuel storage pad. H.4(b)

(Section 1R05.1.b)

Green. The inspectors reviewed a self-revealing, Green finding of EN-DC-115,

Engineering Change Process, involving the failure to maintain adequate design

control measures associated with the installation of the mitigation monitoring

system. On November 8, 2010, a reactor coolant pressure boundary failure

occurred at the skid mounted Online Noble Chemical - Mitigation Monitoring

System pump inside primary containment. The positive displacement sample

pump ejected the pump piston from the housing, resulting in an approximate

7 gpm leak of reactor coolant. The steam leak resulted in a reactor recirculation

system flow control valve lockup (due to hydraulic power unit motor failure) and

approximately 15,000 square feet of contaminated area in the primary

containment structure. The licensee failed to ensure proper validation testing for

the pump prior to installation. Specifically, the licensee did not ensure that the

pump could withstand the operating pressures and temperatures of the system in

- 5 -

Enclosure

which it was installed. The licensee removed the mitigation monitoring system

from service and isolated the skid from the reactor water cleanup system. This

finding was entered into the licensees corrective action program as Condition

Report CR-GGN-2010-07852.

The finding is more than minor because it affects the design control attribute of

the Barrier Integrity Cornerstone to provide reasonable assurance that physical

design barriers protect the public from radionuclide releases caused by accidents

or events. Therefore, using inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 Worksheet for LOCA initiators, the inspectors

concluded that the finding was of very low safety significance (Green) because

the failure of the mitigation monitoring system would not have exceeded technical

specifications limits for identified leakage in the reactor coolant system. This

finding has a crosscutting aspect in the work practices component of the human

performance area; because the licensee failed to adequately oversee the design

of the mitigation monitoring system such that nuclear safety is supported. H.4(c)

(Section 4OA3.2.b)

Cornerstone: Occupational Radiation Safety

Green. The inspectors identified a noncited violation of Technical Specification 5.7.2, resulting from the licensees failure to use a qualified radiation protection

technician to provide direct continuous coverage of work in a locked high

radiation area. The finding was placed into the corrective action program as

Condition Report CR-GGN-2011-01045, and corrective action was being

evaluated.

The failure to use a qualified radiation protection technician to provide direct

continuous coverage of work in a locked high radiation area is a performance

deficiency. The finding was more than minor because it was associated with the

Occupational Radiation Safety Cornerstone attribute (exposure control) of

program and process and affected the cornerstone objective, in that, the failure

to use qualified radiation protection technicians to provide job coverage in a high

radiation area with dose rates in excess of 1000 mrem/hr had the potential to

increase personnel dose. Using the Occupational Radiation Safety Significance

Determination Process, the inspectors determined the finding to have very low

safety significance because: (1) it was not associated with ALARA planning or

work controls, (2) there was no overexposure, (3) there was no substantial

potential for an overexposure, and (4) the ability to assess dose was not

compromised. (Section 2RS01.b)

B.

Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee, have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. These violations and

corrective action tracking numbers (condition report numbers) are listed in

Section 4OA7.

- 6 -

Enclosure

REPORT DETAILS

Summary of Plant Status

Grand Gulf Nuclear Station began the inspection period at full rated thermal power. On January

9, 2011, operators reduced power to 68 percent for a planned control rod sequence exchange

and isolation of the moisture separator reheaters (MSRs) second stage steam to both the A

and B MSRs due to tube leaks in the A MSR. The plant was returned to 96 percent power on

January 10, 2011, which was maximum power level allowed with MSR second stage steam

isolated. On February 18, 2011, operators reduced power to 77 percent for monthly control rod

testing, turbine testing, and to remove B heater drain pump from service in an attempt to repair

a steam leak on the heater drain pump B discharge flange. The plant was returned to 96

percent power on February 19, 2011. On March 11, 2011, operators reduced power to 84

percent power for a planned control rod testing and to remove B heater drain pump from

service in another attempt to repair a steam leak on the heater drain pump B discharge flange.

The plant was returned to 96 percent power on March 12, 2011. On March 23, 2011, operators

reduced power to 93 percent power to remove the B heater drain pump from service again in

another attempt to repair a steam leak on the heater drain pump B pump discharge flange.

The plant was returned to 96 percent power on March 12, 2011. The plant remained at 96

percent power for the remainder of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1

Readiness for Seasonal Extreme Weather Conditions

a.

The inspectors performed a review of the adverse weather procedures for seasonal

extreme low temperatures. The inspectors verified that weather-related equipment

deficiencies identified during the previous year were corrected prior to the onset of

seasonal extremes, and evaluated the implementation of the adverse weather

preparation procedures and compensatory measures for the affected conditions before

the onset of, and during, the adverse weather conditions.

Inspection Scope

During the inspection, the inspectors focused on plant-specific design features and the

procedures used by plant personnel to mitigate or respond to adverse weather

conditions. Additionally, the inspectors reviewed the updated final safety analysis report

and performance requirements for systems selected for inspection and verified that

operator actions were appropriate as specified by plant-specific procedures. Specific

documents reviewed during this inspection are listed in the attachment. The inspectors

also reviewed corrective action program items to verify that plant personnel were

identifying adverse weather issues at an appropriate threshold and entering them into

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Enclosure

their corrective action program in accordance with station corrective action procedures.

The inspectors reviews focused specifically on the following plant systems:

Standby service water

Emergency diesel generators

Plant service water

Fire water pumps and tanks

These activities constitute completion of one readiness for seasonal adverse weather

sample as defined in Inspection Procedure 71111.01-05.

b.

No findings were identified.

Findings

.2

Readiness for Impending Adverse Weather Conditions

a.

Since extreme cold conditions and icing were forecast in the vicinity of the facility for

January 9, 2011, the inspectors reviewed overall preparations/protection for the

expected weather conditions. On January 7, 2011, the inspectors inspected the standby

service water towers because their safety-related functions could be affected as a result

of the extreme cold and icing conditions forecast for the facility. The inspectors observed

space heater operation and weatherized enclosures to ensure operability of affected

systems. The inspectors reviewed licensee procedures and discussed potential

compensatory measures with control room personnel. The inspectors focused on plant

managements actions for implementing the stations procedures for ensuring adequate

personnel for safe plant operation and emergency response would be available.

Specific documents reviewed during this inspection are listed in the attachment.

Inspection Scope

These activities constitute completion of one readiness for impending adverse weather

condition sample as defined in Inspection Procedure 71111.01-05.

b.

No findings were identified.

Findings

1R04 Equipment Alignments (71111.04)

.1

Partial Walkdown

a.

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Inspection Scope

Division II standby service water system during Division I maintenance outage

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Enclosure

Residual heat removal system B during residual heat removal system A

maintenance outage

Residual heat removal system C during residual heat removal system A

maintenance outage

Division II standby diesel generator system during Division I maintenance outage

Standby liquid control system A during standby liquid control system B

maintenance outage

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, technical specification requirements, administrative technical

specifications, outstanding work orders, condition reports, and the impact of ongoing

work activities on redundant trains of equipment in order to identify conditions that could

have rendered the systems incapable of performing their intended functions. The

inspectors also inspected accessible portions of the systems to verify system

components and support equipment were aligned correctly and operable. The

inspectors examined the material condition of the components and observed operating

parameters of equipment to verify that there were no obvious deficiencies. The

inspectors also verified that the licensee had properly identified and resolved equipment

alignment problems that could cause initiating events or impact the capability of

mitigating systems or barriers and entered them into the corrective action program with

the appropriate significance characterization. Specific documents reviewed during this

inspection are listed in the attachment.

These activities constitute completion of five partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

b.

No findings were identified.

Findings

1R05 Fire Protection (71111.05)

Quarterly Fire Inspection Tours

a.

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

Inspection Scope

Division II diesel generator room (1D303)

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Enclosure

Residual heat removal pump and heat exchanger rooms A (1A102 and 1A103)

Residual heat removal pump and heat exchanger rooms B (1A105 and 1A106)

Reactor Core Isolation Pump Room (1A104)

Dry fuel storage pad area (Area 59 the Yard)

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five quarterly fire-protection inspection samples

as defined in Inspection Procedure 71111.05-05.

b.

Findings

Introduction

. The inspectors identified a Green noncited violation of Facility Operating

License Condition 2.C(41), involving the failure to ensure that transient combustible were

not stored in the fire exclusion zone near the independent spent fuel storage installation.

Description

. On January 24, 2011, the inspectors performed a quarterly fire protection

inspection of independent spent fuel storage installation. The inspectors identified a

large air conditioner with combustible material covering it located in the fire exclusion

zone that appeared to be within 60 feet of the dry fuel storage pad. The inspectors

brought this to the attention of the work center senior reactor operator. The work center

senior reactor operator contacted the site fire engineer, who walked down the fire

exclusion zone and determined that the combustible material covering the air conditioner

was within the 60 feet of the dry fuel storage pad, which is in violation of plant procedural

requirements. The inspectors determined through interviews that the material had been

placed there the day before by the maintenance department. The site had the air

conditioner and the covering material removed from the fire exclusion zone to restore

compliance.

The licensee documented this violation in Condition Report CR-GGN-2011-00455. Its

short-term corrective actions included removing the combustible material from the area.

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Enclosure

Analysis. The inspectors determined that the failure to follow fire protection procedures

developed for control of transient combustible material stored near the dry spent fuel

storage pad was a performance deficiency. This finding was more than minor because it

was associated human performance attribute of the Barrier Integrity Cornerstone to

provide reasonable assurance that physical design barriers protect the public from

radionuclide releases caused by accidents or events. Using Manual Chapter 0609,

Appendix F, Fire Protection Significance Determination Process, the inspectors

determined that the finding impacted the fire prevention and administrative controls

category. The inspectors assigned a low degradation rating due to the fact that the

amount of combustible material in the area was minimal. The inspectors concluded that

the finding was of very low safety significance (Green) due to the fact there were no fire

ignition sources in the area. The finding has a crosscutting aspect in the area of human

performance associated with the work practices component because the licensee failed

to effectively communicate expectations regarding storage of combustible material near

the dry fuel storage pad. H.4(b)

Enforcement. Grand Gulf Nuclear Station Facility Operating License Condition 2.C(41)

states, in part, that the plant shall implement and maintain in effect all provisions of the

Fire Protection Program as described in the UFSAR. UFSAR Section 9B,

Administrative Controls, section 9B.6.a, governs the handling and limits the use of

ordinary combustible materials in safety related areas. Fire area 59, defined as the yard,

contains the fire exclusion area next to the dry fuel storage pad and prohibits the storage

of any combustible material in this area. Contrary to this, on January 23, 2011, the

licensee stored combustible material inside the transient combustible exclusion zone

near the dry fuel storage pad. The licensee restored compliance by removing the

material from the area on January 25, 2011. Because the finding was of very low safety

significance (Green) and was documented in the licensees corrective action program as

CR-GGN-2011-0455, this finding is being treated as a noncited violation (NCV)

consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000416/2011002-01; Transient Combustible Stored in the Fire Exclusion Zone

Near the Independent Spent Fuel Storage Installation.

1R06 Flood Protection Measures (71111.06)

a.

The inspectors reviewed the flooding analysis, and plant procedures to assess seasonal

susceptibilities involving internal flooding; reviewed the Updated Final Safety Analysis

Report and corrective action program to determine if licensee personnel identified and

corrected flooding problems; inspected underground bunkers/manholes to verify the

adequacy of sump pumps, level alarm circuits, cable splices subject to submergence,

and drainage for bunkers/manholes; subject to flooding that contain cables whose failure

could disable risk-significant equipment. The inspectors walked down the areas listed

below. Specific documents reviewed during this inspection are listed in the attachment.

Inspection Scope

January 11, 2011, division 1 and 2 standby service water manholes

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Enclosure

These activities constitute completion of one bunker/manhole sample as defined in

Inspection Procedure 71111.06-05.

b.

No findings were identified.

Findings

1R07 Heat Sink Performance (71111.07)

a.

The inspectors reviewed licensee programs, verified performance against industry

standards, and reviewed critical operating parameters and maintenance records for the

Division 1 emergency diesel generator jacket water and lube oil heat exchangers. The

inspectors verified that performance tests were satisfactorily conducted for heat

exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the

periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger

Performance Monitoring Guidelines; the licensee properly utilized biofouling controls;

the licensees heat exchanger inspections adequately assessed the state of cleanliness

of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65,

Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power

Plants. Specific documents reviewed during this inspection are listed in the attachment.

Inspection Scope

These activities constitute completion of one heat sink inspection sample as defined in

Inspection Procedure 71111.07-05.

b.

Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a.

On January 31, 2011, the inspectors observed a crew of licensed operators in the plants

simulator to verify that operator performance was adequate, evaluators were identifying

and documenting crew performance problems and training was being conducted in

accordance with licensee procedures. The inspectors evaluated the following areas:

Inspection Scope

Licensed operator performance

Crews clarity and formality of communications

Crews ability to take timely actions in the conservative direction

Crews prioritization, interpretation, and verification of annunciator alarms

Crews correct use and implementation of abnormal and emergency procedures

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Enclosure

Control board manipulations

Oversight and direction from supervisors

Crews ability to identify and implement appropriate technical specification

actions and emergency plan actions and notifications

The inspectors compared the crews performance in these areas to preestablished

operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed-operator requalification

program sample as defined in Inspection Procedure 71111.11.

b.

No findings were identified.

Findings

1R12 Maintenance Effectiveness (71111.12)

a.

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

Inspection Scope

Appendix R emergency lighting units (Z92)

Control room air conditioning (Z51)

Residual heat removal (E12)

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

Implementing appropriate work practices

Identifying and addressing common cause failures

Scoping of systems in accordance with 10 CFR 50.65(b)

Characterizing system reliability issues for performance

Charging unavailability for performance

Trending key parameters for condition monitoring

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Enclosure

Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)

Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of three quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b.

.1 Failure to Update Available Low Pressure Cooling Injection Loops in the Updated Final

Safety Analysis Report

Findings

Introduction. Inspectors identified a Severity Level IV, noncited violation for the

licensees failure to update the final (updated) safety analysis report in accordance with

10 CFR 50.71(e)(4). Specifically, the licensee failed to update Section 6.3, Emergency

Core Cooling Systems, to appropriately reflect the available emergency core cooling

equipment during shutdown cooling operations in Mode 3.

Description. On February 28, 2011, while reviewing the updated final safety analysis

report for a maintenance effectiveness inspection of the residual heat removal system,

the inspectors determined that Section 6.3.1.1.1.e, Emergency Core Cooling Systems,

states, The ECCS is designed to satisfy all criteria specified in Section 6.3 for any

normal mode of reactor operation. Additionally, Section 6.3.1.1.2.d states, In the event

of a break in a pipe that is part of the reactor coolant pressure boundary, no single active

component failure in the emergency core cooling system shall prevent automatic

initiation and successful operation of less than the following combination of emergency

core cooling system equipment: 1) Three low pressure coolant injection loops, the low

pressure core spray and the automatic depressurization system (i.e., high pressure core

spray failure); 2) Two low pressure coolant injection loops, the high pressure core spray

and the automatic depressurization system (i.e., low pressure core spray diesel

generator failure); and 3) One low pressure coolant injection loop, the low pressure core

spray, the high pressure core spray and automatic depressurization system (i.e., low

pressure coolant injection diesel generator failure).

Procedure 03-1-01-3, Plant Shutdown, Revision 118, Section 6.14 states, When

shutdown cooling is placed in service at less than 135 psig, then the associated

containment spray and low pressure coolant injection systems may be considered

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Enclosure

operable if capable of being manually realigned and not otherwise inoperable.

Inspectors noted that because the residual heat removal system that provides shutdown

cooling in Mode 3 is not available for automatic initiation (must be manually realigned) of

low pressure coolant injection, in the event of a reactor coolant system pipe break, that

the aforementioned statements in Section 6.3 did not appropriately reflect the available

emergency core cooling equipment during shutdown cooling operations. In other words,

the combinations of emergency core cooling equipment available for automatic initiation

would include one less low pressure coolant injection loop.

The licensee entered this issue into their corrective actions program as Condition Report

CR-GGN-2011-01631. The licensee planned to take actions to update the updated final

safety analysis report at the next scheduled revision.

Analysis. The failure of licensing personnel to update the final safety analysis report to

reflect the available low pressure coolant injection loops for automatic initiation during

shutdown cooling operations in Mode 3 was a performance deficiency. This finding was

evaluated using traditional enforcement because it had the potential for impacting the

NRCs ability to perform its regulatory function. The inspectors used the NRC

Enforcement Policy, dated September 30, 2010, to evaluate the significance of this

violation. Consistent with the NRC Enforcement Policy, this finding was determined to

be a Severity Level IV noncited violation. This finding had no crosscutting aspect as it

was associated with a traditional enforcement violation.

Enforcement. Title 10 CFR 50.71(e)(4) requires the final safety analysis report be

updated, at intervals not exceeding 24 months, and states in part, the revisions must

reflect all changes made in the facility or procedures described in the FSAR. Contrary

to the above, licensing personnel failed to update the original revision of the final safety

analysis report to reflect the actual number of low pressure coolant injection loops

available for automatic initiation during shutdown cooling operations in Mode 3.

Because the finding is of very low safety significance and has been entered into the

corrective action program as Condition Report CR-GGN-2011-01631, this violation is

being treated as a noncited violation consistent with the NRC Enforcement Policy:

NCV 0500416/20011002-02, "Failure to Update Available Low Pressure Coolant

Injection Loops in the Updated Final Safety Analysis Report."

.2 Failure to Demonstrate Maintenance Effectiveness of Train B Control Room Air

Conditioner

Introduction. The inspectors identified a Green noncited violation of 10 CFR Part

50.65(a)(2) for the failure to demonstrate that the performance of the train B control

room air conditioner was being effectively controlled through the performance of

appropriate preventive maintenance.

Description. On March 2, 2011, the inspectors performed a maintenance effectiveness

inspection of the control room air conditioning system. Inspectors determined that on

February 3, 2010, the train B control room air conditioner compressor was replaced with

a remanufactured compressor as part of annual preventative maintenance of the

system. On March 27, 2010, the control room air conditioner compressor tripped on low

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Enclosure

usable oil pressure. The licensees investigation revealed that the compressor pencil

strainer was approximately fifty percent covered with unidentified contaminants. Similar

contaminants were identified on the oil sump strainer. The licensee concluded that the

compressor had been installed with contaminants inside the lower half of the

compressor, and subsequently replaced the remanufactured compressor on April 1,

2010, with a newly rebuilt compressor. System engineering did not classify this event as

a maintenance rule functional failure even though operations had declared the train

inoperable and also stated in their operability determination that it could not meet its 30

day mission time.

The train B control room air conditioner compressor subsequently either tripped or failed

to properly cool the control room, due to low usable oil pressure, on three separate

occasions (once in April, once May, and once in June). In response to the June failure,

the licensee performed extensive maintenance on the train B control room air

conditioner compressor, which included installing a five micron suction line filter in the

system. Additionally, all three events were identified as maintenance rule functional

failures attributed to foreign material fouling in the system, which would have resulted in

the performance criteria being exceeded (less than or equal to two maintenance rule

functional failure events or as a repeat functional failure). However, the sites

maintenance rule coordinator informed the inspectors that the first two events in April

and May were not counted toward the criteria because they were from the same cause

as the June event and; therefore, they would all be counted as one failure even thought

the train was returned to service each time after corrective maintenance was performed

and declared operable by operations. Additionally, on June 22, 2010, the train was

declared inoperable due to multiple Freon leaks and was classified as another

maintenance rule functional failure for the train. On August 10, 2010, the licensee

performed a Maintenance Rule (a)(1) evaluation for the subject system and, based on

the presentation to the expert panel by system engineering, the panel only considered

two events as maintenance rule functional failures. System engineering did not count

the one failure in March or consider the two failures in April or May. The expert panel

only considered the failures in June due to low oil pressure and Freon leaks. Therefore

the expert panel concluded that, although the train B control room air conditioner system

had exceeded its established performance criteria for functional failure events, a number

of effective corrective actions had been identified and implemented and additional

corrective actions were not necessary; therefore, the subject system was allowed to

retain its (a)(2) status.

The train B control room air conditioner compressor subsequently either tripped or failed

to properly cool the control room, due to low usable oil pressure, on two separate

occasions (once in September and once in October). The October trip of the subject

system compressor occurred while the train A control room air conditioner was out of

service for routine maintenance. The compressor pencil strainer and sump strainer were

again identified with contaminants on them. The licensee was required to make an

eight-hour report to the NRC and submit a licensee event report due to both trains of

control room air conditioner being inoperable. The licensees root cause analysis failed

to identify that the train B control room air conditioner performance had not been

demonstrated through the performance of appropriate preventative maintenance; nor did

the root cause identify that the licensee failed to set goals and monitor the system as

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Enclosure

required by 10 CFR 50.65(a)(1). The train B control room air conditioner was ultimately

moved into (a)(1) status on February 4, 2011, after the subject compressor again tripped

due to low oil pressure on December 13, 2010. After this trip and upon further

evaluation, the licensee performed an additional corrective action that installed an in line

suction filter with smaller filtering diameter and larger surface area to remove foreign

material from the system. They also modified the operator rounds to obtain daily

readings of differential pressure across this new filter and through calculation,

determined a differential pressure necessary for the filter to be changed out and the unit

to be inspected for foreign materials.

The licensee entered this issue into their corrective actions program as Condition Report

CR-GGN-2011-01623. From installation of the new inline suction filter to the conclusion

of the inspection period, no additional trips of train B control room air conditioning have

occurred.

Analysis. The inspectors determined that the failure to demonstrate that the

performance of the train B control room air conditioner was being effectively controlled

through the performance of appropriate preventive maintenance was a performance

deficiency. The finding was more than minor because it was associated with the

equipment performance attribute of the Mitigating Systems Cornerstone and adversely

affected the cornerstone objective to ensure the availability, reliability, and capability of

systems that respond to initiating events to prevent undesirable consequences.

Inspectors performed a Phase 1 screening, in accordance with Inspection Manual

Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of

Findings, and determined that the finding was of very low safety significance (Green)

because it did not result in a loss of system safety function since the train A control room

air conditioner remained operable. This finding had a crosscutting aspect in the area of

human performance associated with the decision making component because licensee

personnel failed to make appropriate safety-significant or risk-significant decisions to

address the multiple failures of the train B CRAC compressor. H.1(a)

Enforcement. Title 10 CFR 50.65(a)(2), states, in part, that monitoring as specified in

paragraph (a)(1) of this section is not required where it has been demonstrated that the

performance or condition of a structure, system, or component is being effectively

controlled through the performance of appropriate preventative maintenance, such that

the structure, system, or component remains capable of performing its intended

function. Contrary to the above, from March 2010 to February 2011, the licensee failed

to demonstrate that the performance of the train B control room air conditioning system

was effectively controlled through the performance of appropriate preventative

maintenance. This finding was entered into the licensees corrective action program as

Condition Report CR-GGN-2011-01623. Because this finding was determined to be of

very low safety significance and was entered into the licensees corrective action

program, this violation is being treated as a noncited violation consistent with the NRC

Enforcement Policy: NCV 05000285/2011002-03, Failure to Demonstrate Maintenance

Effectiveness of Train B Control Room Air Conditioner.

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Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

Inspection Scope

On January 9, 2011, during an ice storm requiring the plant to enter a yellow risk

condition and enter their off normal event procedure for severe weather.

On February 3, 2011, during an ice storm requiring the plant to enter a yellow risk

condition and enter their off normal event procedure for severe weather. The

weather required the site to cancel work and monitor their safety related standby

service water system for icing conditions.

On February 9, 2011, during a winter storm, while a divisions 1 diesel generator

and residual heat removal A were out for planned maintenance outage requiring

the plant to enter orange risk.

On February 28, 2011, during the accidental unearthing of energized plant

service water pump cables, no consequence to the plant but resulted in work

stoppage and evaluation of risk status for the site.

On March 8-9, 2011, with an emergent issue with the division 1 diesel generator

and a tornado watch issued for the area requiring the plant to enter yellow risk.

The site entered their severe weather off normal procedure; this procedure

required the site to secure from half scram surveillances.

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five emergent work control inspection samples

as defined in Inspection Procedure 71111.13-05.

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Enclosure

b.

No findings were identified.

Findings

1R15 Operability Evaluations (71111.15)

a.

The inspectors reviewed the following issues:

Inspection Scope

Division 3 high pressure core spray diesel generator outside air fan temperature

switch fluctuating

Train A standby service water drift eliminator support base plate corrosion and

missing brass bolts

Train A standby service water valve P41-F299A flange degradation

Residual heat removal equipment area temperature high/inoperable due to

temperature switch

Site fire truck inoperable

Division 1 diesel generator auxiliary oil pump not obtaining procedural pressures

during pre-lube prior to surveillance run

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and UFSAR to

the licensee personnels evaluations to determine whether the components or systems

were operable. Where compensatory measures were required to maintain operability,

the inspectors determined whether the measures in place would function as intended

and were properly controlled. The inspectors determined, where appropriate,

compliance with bounding limitations associated with the evaluations. Additionally, the

inspectors also reviewed a sampling of corrective action documents to verify that the

licensee was identifying and correcting any deficiencies associated with operability

evaluations. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of six operability evaluations inspection samples

as defined in Inspection Procedure 71111.15-04

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Enclosure

b.

No findings were identified.

Findings

1R18 Plant Modifications (71111.18)

a.

To verify that the safety functions of important safety systems were not degraded, the

inspectors reviewed the following temporary modifications:

Inspection Scope

Temporary Modification for RWCU A/B Leak Detection (EC 22625 & EC 22635)

Temporary Modification to install bypass signals for B first stage Pressure

Sensor (EC22768)

The inspectors reviewed the temporary modifications and the associated safety-

evaluation screening against the system design bases documentation, including the

updated final safety analysis report and the technical specifications, and verified that the

modification did not adversely affect the system operability/availability. The inspectors

also verified that the installation and restoration were consistent with the modification

documents and that configuration control was adequate. Additionally, the inspectors

verified that the temporary modification was identified on control room drawings,

appropriate tags were placed on the affected equipment, and licensee personnel

evaluated the combined effects on mitigating systems and the integrity of radiological

barriers.

These activities constitute completion of two samples for temporary plant modifications

as defined in Inspection Procedure 71111.18-05.

b.

No findings were identified.

Findings

1R19 Postmaintenance Testing (71111.19)

a.

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

Inspection Scope

For standby liquid B after a maintenance outage

For reactor protection motor generator B after required maintenance

For residual heat removal system A after a maintenance outage

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Enclosure

For standby service water system A after a maintenance outage

For division 1 diesel generator after a maintenance outage

For high pressure core spray minimum flow valve 1E22-F012 after corrective

maintenance

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the UFSAR,

10 CFR Part 50 requirements, licensee procedures, and various NRC generic

communications to ensure that the test results adequately ensured that the equipment

met the licensing basis and design requirements. In addition, the inspectors reviewed

corrective action documents associated with postmaintenance tests to determine

whether the licensee was identifying problems and entering them in the corrective action

program and that the problems were being corrected commensurate with their

importance to safety. Specific documents reviewed during this inspection are listed in

the attachment.

These activities constitute completion of six postmaintenance testing inspection samples

as defined in Inspection Procedure 71111.19-05.

b.

No findings were identified.

Findings

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors reviewed the UFSAR, procedure requirements, and technical

specifications to ensure that the surveillance activities listed below demonstrated that the

systems, structures, and/or components tested were capable of performing their

intended safety functions. The inspectors either witnessed or reviewed test data to

verify that the significant surveillance test attributes were adequate to address the

following:

Preconditioning

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Enclosure

Evaluation of testing impact on the plant

Acceptance criteria

Test equipment

Procedures

Test data

Testing frequency and method demonstrated technical specification operability

Test equipment removal

Restoration of plant systems

Updating of performance indicator data

Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

Reference setting data

Annunciators and alarms setpoints

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

On January 7, 2011, reactor coolant system leakage detection surveillance

On February 4, 2011, inservice test of residual heat removal system B quarterly

On February 23, 2011, reactor coolant routine chemistry surveillance

On March 2, 2011, fuel handling area ventilation exhaust radiation monitor time

response test

On March 10, 2011, division 1 diesel generator monthly surveillance

On March 18, 2011, division 3 diesel generator monthly surveillance

On March 20-21, 2011, functional checks with reactor core isolation cooling

valves at the remote shutdown panel

Specific documents reviewed during this inspection are listed in the attachment.

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Enclosure

These activities constitute completion of seven surveillance (one reactor coolant system

leakage detection, one inservice test, and five routine tests) testing inspection samples

as defined in Inspection Procedure 71111.22-05.

b.

No findings were identified.

Findings

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06)

.1

Emergency Preparedness Drill Observation

a.

The inspectors evaluated the conduct of a routine licensee emergency drill on March 3,

2011, to identify any weaknesses and deficiencies in classification, notification, and

protective action recommendation development activities. The inspectors observed

emergency response operations in the simulator control room and emergency

operations facility to determine whether the event classification, notifications, and

protective action recommendations were performed in accordance with procedures. The

inspectors also attended the licensee drill critique to compare any inspector-observed

weakness with those identified by the licensee staff in order to evaluate the critique and

to verify whether the licensee staff was properly identifying weaknesses and entering

them into the corrective action program. As part of the inspection, the inspectors

reviewed the drill package and other documents listed in the attachment.

Inspection Scope

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.06-05.

b.

No findings were identified.

Findings

2.

RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

2RS01 Radiological Hazard Assessment and Exposure Controls (71124.01)

a.

Inspection Scope

This area was inspected to: (1) review and assess licensees performance in assessing

the radiological hazards in the workplace associated with licensed activities and the

implementation of appropriate radiation monitoring and exposure control measures for

both individual and collective exposures, (2) verify the licensee is properly identifying

and reporting Occupational Radiation Safety Cornerstone performance indicators, and

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Enclosure

(3) identify those performance deficiencies that were reportable as a performance

indicator and which may have represented a substantial potential for overexposure of

the worker.

The inspectors used the requirements in 10 CFR Part 20, the technical specifications,

and the licensees procedures required by technical specifications as criteria for

determining compliance. During the inspection, the inspectors interviewed the radiation

protection manager, radiation protection supervisors, and radiation workers. The

inspectors performed walkdowns of various portions of the plant, performed independent

radiation dose rate measurements and reviewed the following items:

Performance indicator events and associated documentation reported by the

licensee in the Occupational Radiation Safety Cornerstone

The hazard assessment program, including a review of the licenses evaluations

of changes in plant operations and radiological surveys to detect dose rates,

airborne radioactivity, and surface contamination levels

Instructions and notices to workers, including labeling or marking containers of

radioactive material, radiation work permits, actions for electronic dosimeter

alarms, and changes to radiological conditions

Programs and processes for control of sealed sources and release of potentially

contaminated material from the radiologically controlled area, including survey

performance, instrument sensitivity, release criteria, procedural guidance, and

sealed source accountability

Radiological hazards control and work coverage, including the adequacy of

surveys, radiation protection job coverage, and contamination controls; the use of

electronic dosimeters in high noise areas; dosimetry placement; airborne

radioactivity monitoring; controls for highly activated or contaminated materials

(non-fuel) stored within spent fuel and other storage pools; and posting and

physical controls for high radiation areas and very high radiation areas

Radiation worker and radiation protection technician performance with respect to

radiation protection work requirements

Audits, self-assessments, and corrective action documents related to radiological

hazard assessment and exposure controls since the last inspection

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.01-05.

b.

Findings

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Enclosure

Introduction. The inspectors identified a Green, noncited violation of Technical

Specification 5.7.2, resulting from the licensees failure to use a qualified radiation

protection technician to provide direct continuous coverage of work in a locked high

radiation area.

Description. The inspectors reviewed Condition Report CR-GGN-2011-00655, which

documented the identification by Cooper Nuclear Station that a contractor seeking

employment as a radiation protection technician did not meet ANSI 18.1 requirements.

The finding, documented February 2, 2011, was discussed with Entergy sites during a

teleconference. Then, Grand Gulf Nuclear Station determined the individual had been

employed as a radiation protection technician at Grand Gulf Nuclear Station during

Refueling Outage 17, conducted in April and May 2010. In response, Grand Gulf

Nuclear Station reviewed the radiation surveys performed by the individual (from April 15

through May 13, 2010), concluded the surveys contained data comparable with that

documented in other surveys in the same areas under similar conditions, and closed the

condition report on February 8, 2011. The inspectors reviewed the radiation survey

records included in the condition report and noted something the licensee had not

addressed. On April 27, 2010, the individual had provided job coverage for work in a

locked high radiation area (an area with dose rates greater than 1000 mrem/hour).

Survey GG-1004-0660 identified the work area as the 128-foot auxiliary pipe chase,

above the reactor water cleanup pump rooms. Since the individual used by the licensee

to provide job coverage and surveillance in a locked high radiation area was not a

qualified radiation protection technician, the inspectors identified this as a performance

deficiency.

Analysis. The failure to use a qualified radiation protection technician to provide direct

continuous coverage of work in a locked high radiation area is a performance deficiency.

The finding was more than minor because it was associated with the Occupational

Radiation Safety Cornerstone attribute (exposure control) of program and process and

affected the cornerstone objective, in that, the failure to use qualified radiation protection

technicians to provide job coverage in a high radiation area with dose rates in excess of

1000 mrem/hr had the potential to increase personnel dose. Using the Occupational

Radiation Safety Significance Determination Process, the inspectors determined the

finding to have very low safety significance because: (1) it was not associated with

ALARA planning or work controls, (2) there was no overexposure, (3) there was no

substantial potential for an overexposure, and (4) the ability to assess dose was not

compromised. The inspectors identified no cross-cutting aspect associated with this

finding.

Enforcement. Technical Specification 5.7.2, controls for high radiation areas with dose

rates greater than 1000 mrem/hour, consists of all the controls for high radiation areas

(Technical Specification 5.7.1) plus it requires doors to the area remain locked except

during periods of access by personnel under an approved radiation work permit that

shall specify the dose rate levels in the immediate work areas and the maximum

allowable stay times for individuals in those areas. In lieu of the stay time specification

for the radiation work permit, direct or remote continuous surveillance may be made by

personnel qualified in radiation protection procedures to provide positive exposure

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Enclosure

control over the activities being performed within the area. Contrary to the above, during

work in an area with dose rates greater than 1000 mrem/hour on April 27, 2010, in lieu of

the stay time specification for the radiation work permit, direct or remote surveillance

was not made by personnel qualified in radiation protection procedures to provide

positive exposure control over the activities being performed within the area. Instead, an

unqualified person was assigned to provide surveillance of a locked high radiation on

April 27, 2010. The licensee initiated Condition Report CR-GGN-2011-01045 to

document the fact that it failed to identify this performance deficiency as part of the

review associated with the closure of Condition Report CR-GGN-2011-00655.

Because the violation was of very low safety significance and it was entered into the

licensees corrective action program, the violation is being treated as a noncited

violation, consistent with the enforcement policy. NCV 05000416/2011002-04, Failure

to Use a Qualified Radiation Protection Technician to Provide Direct Continuous

Coverage of Work in a Locked High Radiation Area.

2RS02 Occupational ALARA Planning and Controls (71124.02)

a.

Inspection Scope

This area was inspected to assess performance with respect to maintaining occupational

individual and collective radiation exposures as low as is reasonably achievable

(ALARA). The inspectors used the requirements in 10 CFR Part 20, the technical

specifications, and the licensees procedures required by technical specifications as

criteria for determining compliance. During the inspection, the inspectors interviewed

licensee personnel and reviewed the following items:

Site-specific ALARA procedures and collective exposure history, including the

current 3-year rolling average, site-specific trends in collective exposures, and

source-term measurements

ALARA work activity evaluations/postjob reviews, exposure estimates, and

exposure mitigation requirements

The methodology for estimating work activity exposures, the intended dose

outcome, the accuracy of dose rate and man-hour estimates, and intended

versus actual work activity doses and the reasons for any inconsistencies

Records detailing the historical trends and current status of tracked plant source

terms and contingency plans for expected changes in the source term due to

changes in plant fuel performance issues or changes in plant primary chemistry

Radiation worker and radiation protection technician performance during work

activities in radiation areas, airborne radioactivity areas, or high radiation areas

Audits, self-assessments, and corrective action documents related to ALARA

planning and controls since the last inspection

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Enclosure

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of the one required sample as defined in

Inspection Procedure 71124.02-05.

b.

Findings

No findings were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1

Data Submission Issue

a.

The inspectors performed a review of the performance indicator data submitted by the

licensee for the fourth Quarter 2010 performance indicators for any obvious

inconsistencies prior to its public release in accordance with Inspection Manual

Chapter 0608, Performance Indicator Program.

Inspection Scope

This review was performed as part of the inspectors normal plant status activities and,

as such, did not constitute a separate inspection sample.

b.

No findings were identified.

Findings

.2

Unplanned Scrams per 7000 Critical Hours (IE01)

a.

The inspectors sampled licensee submittals for the unplanned scrams per 7000 critical

hours performance indicator for the period from the first quarter 2010 through the fourth

quarter 2010. To determine the accuracy of the performance indicator data reported

during those periods, the inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.

The inspectors reviewed the licensees operator narrative logs, condition reports, event

reports, and NRC integrated inspection reports for the period of January 2010 through

December 2010 to validate the accuracy of the submittals. The inspectors also reviewed

the licensees condition report database to determine if any problems had been identified

with the performance indicator data collected or transmitted for this indicator and none

were identified. Specific documents reviewed are described in the attachment to this

report.

Inspection Scope

These activities constitute completion of one unplanned scrams per 7000 critical hours

sample as defined in Inspection Procedure 71151-05.

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Enclosure

b.

No findings were identified.

Findings

.3

Unplanned Scrams with Complications (IE02)

a.

The inspectors sampled licensee submittals for the unplanned scrams with

complications performance indicator for the period from first quarter 2010 through the

fourth quarter 2010. To determine the accuracy of the performance indicator data

reported during those periods, the inspectors used definitions and guidance contained in

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6. The inspectors reviewed the licensees operator narrative logs, condition

reports, event reports, and NRC integrated inspection reports for the period of January

2010 through December 2010 to validate the accuracy of the submittals. The inspectors

also reviewed the licensees condition report database to determine if any problems had

been identified with the performance indicator data collected or transmitted for this

indicator and none were identified. Specific documents reviewed are described in the

attachment to this report.

Inspection Scope

These activities constitute completion of one unplanned scrams with complications

sample as defined in Inspection Procedure 71151-05.

b.

No findings were identified.

Findings

.4

Unplanned Power Changes per 7000 Critical Hours (IE03)

a.

The inspectors sampled licensee submittals for the unplanned power changes per 7000

critical hours performance indicator for the period from first quarter 2010 through the

fourth quarter 2010. To determine the accuracy of the performance indicator data

reported during those periods, the inspectors used definitions and guidance contained in

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6. The inspectors reviewed the licensees operator narrative logs, condition

reports, event reports, and NRC integrated inspection reports for the period of January

2010 through December 2010 to validate the accuracy of the submittals. The inspectors

also reviewed the licensees condition report database to determine if any problems had

been identified with the performance indicator data collected or transmitted for this

indicator and none were identified. Specific documents reviewed are described in the

attachment to this report.

Inspection Scope

These activities constitute completion of one unplanned transients per 7000 critical

hours sample as defined in Inspection Procedure 71151-05.

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Enclosure

b.

No findings were identified.

Findings

.5

Occupational Exposure Control Effectiveness (OR01)

a.

Inspection Scope

The inspectors reviewed performance indicator data for the second quarter of 2010

through the fourth quarter of 2010. The objective of the inspection was to determine the

accuracy and completeness of the performance indicator data reported during these

periods. The inspectors used the definitions and clarifying notes contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,

as criteria for determining whether the licensee was in compliance.

The inspectors reviewed corrective action program records associated with high

radiation area (greater than 1 rem/hr) and very high radiation area non-conformances.

The inspectors reviewed radiological, controlled area exit transactions greater than

100 mrem. The inspectors also conducted walkdowns of high radiation areas (greater

than 1 rem/hr) and very high radiation area entrances to determine the adequacy of the

controls of these areas.

These activities constitute completion of the occupational exposure control effectiveness

sample as defined in Inspection Procedure 71151-05.

b.

Findings

No findings were identified.

.6

Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (PR01)

a.

Inspection Scope

The inspectors reviewed performance indicator data for the second quarter of 2010

through the fourth quarter of 2010. The objective of the inspection was to determine the

accuracy and completeness of the performance indicator data reported during these

periods. The inspectors used the definitions and clarifying notes contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6,

as criteria for determining whether the licensee was in compliance.

The inspectors reviewed the licensees corrective action program records and selected

individual annual or special reports to identify potential occurrences such as

unmonitored, uncontrolled, or improperly calculated effluent releases that may have

impacted offsite dose.

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Enclosure

These activities constitute completion of the radiological effluent technical

specifications/offsite dose calculation manual radiological effluent occurrences sample

as defined in Inspection Procedure 71151-05.

b.

Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1

Routine Review of Identification and Resolution of Problems

a.

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees

corrective action program at an appropriate threshold, that adequate attention was being

given to timely corrective actions, and that adverse trends were identified and

addressed. The inspectors reviewed attributes that included the complete and accurate

identification of the problem; the timely correction, commensurate with the safety

significance; the evaluation and disposition of performance issues, generic implications,

common causes, contributing factors, root causes, extent of condition reviews, and

previous occurrences reviews; and the classification, prioritization, focus, and timeliness

of corrective actions. Minor issues entered into the licensees corrective action program

because of the inspectors observations are included in the attached list of documents

reviewed.

Inspection Scope

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure, they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

No findings were identified.

Findings

.2

Daily Corrective Action Program Reviews

a.

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

Inspection Scope

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Enclosure

items entered into the licensees corrective action program. The inspectors

accomplished this through review of the stations daily corrective action documents.

The inspectors performed these daily reviews as part of their daily plant status

monitoring activities and, as such, did not constitute any separate inspection samples.

b.

No findings were identified.

Findings

.3

Selected Issue Follow-up Inspection

a.

During a review of items entered in the licensees corrective action program, the

inspectors recognized CR-GGN- 2009-05879 a corrective action item documenting

temperature switches for safety related ventilation system. The inspectors reviewed that

item as described in Inspection Procedure 71152.02 to verify, in part, licensee evaluation

and disposition of operability and reportability issues; consideration of extent of condition

and cause, generic implications, common cause, and previous occurrences;

classification and prioritization of the problems resolution commensurate with the safety

significance; and identification of corrective actions that were appropriately focused to

correct the problem.

Inspection Scope

These activities constitute completion of one in-depth problem identification and

resolution sample as defined in Inspection Procedure 71152-05.

b.

No findings were identified.

Findings

4OA3 Event Follow-up (71153)

.1

(Closed) LER 05000416/2010-002-00, Control Room Air Conditioning Inoperability -

Loss of Both Trains

a.

On October 14, 2010, while operating at approximately 100 percent power, the train B

control room air conditioner subsystem tripped on low oil pressure while the train A

control room air conditioner subsystem was out of service for maintenance. The control

room temperature increased and actions were taken to maintain control room

temperatures below the technical specification limit of 90 degrees Fahrenheit. The two

control room air conditioning subsystems were inoperable for 64 hours7.407407e-4 days <br />0.0178 hours <br />1.058201e-4 weeks <br />2.4352e-5 months <br /> and 24 minutes

until the train A control room air conditioner was declared operable.

Inspection Scope

The three possible failure mechanisms that the licensee identified in their root cause

evaluation were 1) the intermittent failure of the low oil differential pressure switch, 2) the

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Enclosure

intermittent failure of one or more loading/unloading mechanisms, and 3) one or more of

the temperature control valves were in an open condition or in a more than desired open

position. The licensee also identified a contributing cause of failure to exclude foreign

material during maintenance activities on the train B control room air conditioner.

Inspectors reviewed the circumstances surrounding the event, the licensees response

to the event, and the licensees corrective actions to preclude repetition. Documents

reviewed as part of this inspection are listed in the attachment. The enforcement

aspects of this finding are discussed in this section and in Section 1R12. This LER is

closed.

b.

Findings

Introduction. The inspectors reviewed a self-revealing, Green noncited violation of 10

CFR Part 50, Appendix B, Criterion XVI, Corrective Action, after the licensee failed to

determine the cause and prevent recurrence of a significant condition adverse to quality

associated with the train B control room air conditioner compressor tripping due to low oil

pressure.

Description. On October 14, 2010, the train B control room air conditioner subsystem

tripped on low oil pressure while the train A control room air conditioner subsystem was

out of service for maintenance. The control room temperature increased, and actions

were taken to maintain control room temperatures below the technical specification limit

of 90 degrees Fahrenheit. The licensee determined that the event (i.e., one subsystem

inoperable and unavailable for maintenance while the other subsystem was inoperable

due to a trip) was reportable to the NRC. The two control room air conditioning

subsystems were inoperable for 64 hours7.407407e-4 days <br />0.0178 hours <br />1.058201e-4 weeks <br />2.4352e-5 months <br /> and 24 minutes until the train A control room

air conditioner was declared operable. This was a significant condition because it

rendered technical specification required equipment inoperable.

The licensees corrective actions to address the event involved performing a root cause

evaluation. The licensee concluded that the three possible failure mechanisms were 1)

an intermittent failure of low oil differential pressure switch, 2) an intermittent failure of

one or more loading/unloading mechanisms, and 3) failure of one or more thermal

expansion valves. The licensee also concluded that a contributing cause of the event

was the failure to exclude foreign material during maintenance activities of the system.

The licensee addressed each of the possible root causes, as well as the contributing

cause, since a single root cause could not be determined. The corrective action for the

three probable root causes included 1) ensuring that only original differential pressure

switches are used (or a suitable equivalent) for replacement; 2) revising planned

maintenance tasks to included instructions for the loader/unloader disassembly,

inspection and reassembly; 3) revising tasks for compressor A and B rebuilds; and 4)

revising compressor preventative maintenance tasks to record the degree of superheat

for each thermal expansion valve.

Despite the corrective actions implemented by the licensee, the train B control room air

conditioner compressor again tripped on December 13, 2010, due to low oil pressure.

After this trip and upon further evaluation, the licensee performed an additional

corrective action that installed an inline suction filter with smaller filtering diameter and

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Enclosure

larger surface area to remove foreign material from the system. The licensee also

modified the operator rounds to obtain daily readings of differential pressure across this

new filter and through calculation, determined a differential pressure necessary to

change the filter. The condition report that documented the December 13th event was

closed to the corrective actions associated with the October 14th compressor trip and the

new corrective action associated with the newly installed in line suction filter.

The licensee entered this event into their corrective actions program as condition report

CR-GGN-2010-07315. Since the use of the new inline suction filter, they have not had

any additional trips of the control room air conditioning B. The April 2011 inspection

showed that the filter had reduced foreign material on the compressor suction strainer by

40 percent from the March 2011 inspection. Also in May 2011, the licensee plans to

boroscope the evaporation section of the air conditioner to search for any other foreign

material.

Analysis. The inspectors determined that the failure to take corrective actions to prevent

recurrence of the train B control room air conditioner compressor tripping due to low oil

pressure was a performance deficiency. This finding was more than minor because it

was associated with the equipment performance attribute of the Mitigating Systems

Cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Using Inspection Manual Chapter 0609, "Significance

Determination Process," Phase 1 worksheets, the inspectors determined that a Phase 2

estimate was required because the finding represented a loss of system safety function.

The plant-specific risk informed notebook does not include the evaluation of risk caused

by the loss of cooling to the main control room. Therefore, the senior reactor analyst

conducted a Phase 3 analysis.

The analyst noted that understanding the risk affect of control room chillers required a

review of the following items:

Loss of offsite power frequency (LOOP): Several alternative methods of cooling

control room equipment are available provided offsite power is available.

Therefore, the dominant risk impact of essential chillers is during a loss of offsite

power. The loss of offsite power frequency documented in the plant-specific

SPAR model is 3.59 x 10-2/year.

Loss of the opposite train probability (PCH-A): The performance deficiency only

affected Train B CRAC. Therefore, the Train A would still be available to cool the

main control room. The generic failure probability for a single train of safety-

related equipment is approximately 3 x 10-2/demand.

Exposure Period (EXP): Although the Train B CRAC system was placed in

service without correcting the failure mechanism on November 1, 2010, the

chiller continued to be utilized and run for much of the time until failure on

December 13, 2010. The analyst noted that the chiller ran from November 12

until it failed on December 13, 2010. Therefore, the time that the chiller was

actually unavailable to perform its 24-hour risk significant mission time was

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Enclosure

about 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> (the last 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of its run and the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> it took to repair).

This gave an exposure time of 2 days.

Conditional Core Damage Probability (CCDP): In the worst case failure of

control room air conditioning would result in main control room abandonment.

The generic CCDP for shutting the reactor down from outside the main control

room is approximately 0.1.

The analyst determined that a bounding assessment of the change in core damage

frequency (CDF), can be calculated as follows:

CDF = LOOP * PCH-A * EXP * CCDP

= 3.59 x 10-2/year * 3 x 10-2/demand * 2 days/365 days/year * 0.1

= 5.9 x 10-7

Based on the above bounding analysis, the analyst determined that the change in core

damage frequency result was 5.9 x 10-7. This noncited violation was therefore

determined to be of very low safety significance (Green). This finding had a crosscutting

aspect in the area of problem identification and resolution associated with the corrective

action program component because licensee personnel failed to thoroughly evaluate the

multiple failures of the train B control room air conditioner compressor. P.1(c)

Enforcement. Title 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action,

states, in part, that in the case of a significant condition adverse to quality, measures

shall assure that the cause of the condition is determined and corrective action taken to

preclude repetition. Contrary to the above, plant personnel did not implement corrective

actions to preclude repetition of a significant condition adverse to quality associated with

the tripping of the train B control room air conditioning compressor due to low oil

pressure. Specifically, on December 13, 2010, the train B control room air conditioner

compressor tripped due to low oil pressure after the licensee had a performed a root

cause analysis to identify the cause and prevent recurrence of the compressor tripping

due to low oil pressure. Because the finding was of very low safety significance and has

been entered into the corrective action program as Condition Report CR-GGN-2010-

07315, this violation is being treated as a noncited violation, consistent with the NRC

Enforcement Policy. NCV 05000416/2011002-05, Failure to Prevent Recurrence of

Control Room Air Conditioner Compressor Tripping Due to Low Oil Pressure.

.2

Steam Leak in the Containment

a.

On November 8, 2010, the inspectors responded to the control room to observe operator

response to a steam leak in containment. The newly installed mitigation monitoring

system positive displacement pump ejected the cylinder causing an approximate seven

gallons per minute reactor coolant leak. The inspectors observed operator actions,

control room briefs and overall plant response to the event. The inspectors also

Inspection Scope

- 34 -

Enclosure

observed control room indications used to identify abnormal conditions in the

containment building. Documents reviewed for this inspection are listed in the

attachment.

b. Findings

Introduction. The inspectors reviewed a self-revealing, Green finding of EN-DC-115,

Engineering Change Process, involving the failure to maintain adequate design control

measures associated with the installation of the mitigation monitoring system.

Description. On November 8, 2010, at approximately 5:30 am, a reactor coolant

pressure boundary failure occurred at the skid mounted Online Noble Chemical -

Mitigation Monitoring System pump inside primary containment. The positive

displacement sample pump ejected the pump piston from the housing resulting in an

approximate 7 gpm leak of reactor coolant. The leak was not detected for approximately

4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />, resulting in the release of approximately 2,000 gallons of reactor coolant

which flashed directly to steam. The steam leak resulted in a reactor recirculation system

flow control valve lockup (due to HPU motor failure) and approximately 15,000 square

feet of contaminated area in the primary containment structure.

The inspectors reviewed the mitigation monitoring system modification documentation

and found that the design documentation did not appropriately address the design

requirements for the installation of the mitigation monitoring system pump. The licensee

failed to ensure proper validation testing for the pump prior to installation in the plant.

Specifically, they did not ensure that the pump would be able to withstand the system

operating pressures and temperatures in which it was installed. They failed to validate

the design, which had a single point vulnerability, that resulted in the piston injecting

from the pump and caused the leakage and contamination of the containment. In

addition, the inspectors reviewed the root cause analysis of the event and found that the

licensee failed to apply the appropriate oversight of the engineering vendor due to

weaknesses in the procedure EN-DC-114, "Vendor Quality Management/Oversight."

The licensee entered this event into their corrective actions program as condition report

CR-GGN-2010-07852. The licensee has currently removed the mitigation monitoring

system pump from the plant, and isolated the mitigation monitoring system skid from the

reactor water cleanup system. They are evaluating the design to make appropriate

changes to ensure a repeat of this event will not occur.

Analysis. The failure to implement adequate design control measures for modifications

to the plant, which impacted the reactor coolant pressure boundary, is a performance

deficiency. Specifically procedure EN-DC-115, Engineering Change Process, step

5.1[1], requires during the engineering change development a choice of new technology

or application is an error precursor which will need to have defensive functions built into

the design, testing and maintenance, including developing in-house expertise. Contrary

to this, the engineering change package that implemented this design change failed to

ensure proper validation testing was performed prior to installation in the plant. The

finding is more than minor because it affects the design control attribute of the Barrier

Integrity Cornerstone to provide reasonable assurance that physical design barriers

- 35 -

Enclosure

protect the public from radionuclide releases caused by accidents or events. Therefore,

using inspection Manual Chapter 0609, "Significance Determination Process," Phase 1

Worksheet for LOCA initiators, the inspectors concluded that the finding was of very low

safety significance (Green) because the failure of the mitigation monitoring system would

not have exceeded technical specifications limits for identified leakage in the reactor

coolant system. This finding has a crosscutting aspect in the area of human

performance associated with the work practices component because the licensee failed

to adequately oversee the design of the mitigation monitor system such that nuclear

safety is supported. H.4(c)

Enforcement. No violation of regulatory requirements occurred. This finding was

entered into the licensees corrective action program as CR-GGN-2010-07852, and is

identified as: FIN 05000416/2011002-06, Inadequate Design Control for the Mitigation

Monitoring System Modification.

4OA5 Other Activities

1.

(Closed) Temporary Instruction (TI) 2515/179, Verification of Licensee Responses to

NRC Requirement for Inventories of Materials Tracked in the National Source Tracking

System Pursuant to Title 10, Code of Federal Regulations, Part 20.2207 (10 CFR

20.2207)

a.

Inspection Scope

An NRC inspection was performed to confirm that the licensee has reported their initial

inventories of sealed sources pursuant to 10 CFR 20.2207 and to verify that the National

Source Tracking System database correctly reflects the Category 1 and 2 sealed

sources in custody of the licensee. Inspectors interviewed personnel and performed the

following:

Reviewed the licensees source inventory

Verified the presence of any Category 1 or 2 sources

Reviewed procedures for and evaluated the effectiveness of storage and handling

of sources

Reviewed documents involving transactions of sources

Reviewed adequacy of licensee maintenance, posting, and labeling of nationally

tracked sources

b.

Findings

While comparing the National Source Tracking System database information, the

Licensees information submittal, and original source certificates, the inspector noted

that the licensee erroneously reported information for one of the four sources meeting

the reporting criteria. The licensee used original leak test data and submitted the wrong

- 36 -

Enclosure

serial number and activity date for the source. The licensee reviewed all relevant data

and submitted corrected documents within the five business days allowed by

10 CFR 20.2207(g). This finding was considered as an administrative error and of minor

safety significance.

4OA6 Meetings

Exit Meeting Summary

On February 18, 2011, the inspectors presented the results of the radiation safety inspections to

Mr. J. Browning, General Plant Manager, and other members of the licensee staff. The licensee

acknowledged the issues presented. The inspectors asked the licensee whether any materials

examined during the inspection should be considered proprietary. No proprietary information

was identified.

On April 14, 2011, the inspectors presented the inspection results to M. Perito, Site Vice-

President Operations and other members of the licensee staff. The licensee acknowledged the

issues presented. The inspector asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section 2.3.2 of the NRC

Enforcement Policy for being dispositioned as noncited violations.

.1

Technical Requirements Manual (TRM) section 6.2.1 requires that fire detection

instrumentation for each fire detection zone shall be operable and if the required

detection system is inoperable an hourly fire watch must be established. Contrary to

this, on February 9, 2011 the licensee identified that fire detection instrumentation for fire

zone 2-12 had been left in the non-audible alarm for the main control room on the fire

computer when the limiting condition for operations was cleared on December 8, 2010

when zone was returned to operable status. The control room supervisor on February 9,

2011, discovered this condition when entering a fire-limiting condition for operation for

the division 1 diesel generator room to allow welding. The licensee determined that it

had been in non-audible status from December 8, 2010, through February 9, 2011. This

issue was documented in the licensees corrective action program in condition report

CR-GGN-2011-00851. The senior reactor analyst from region IV performed a bounding

evaluation of the change in risk caused by this condition. According to the Grand Gulf

Updated Final Safety Analysis Report, Fire Zone 2-12 only contains Division I

equipment. A fire that consumed the equipment in the area could not result in a loss of

offsite power or other unplanned transient. Given the ignition frequency of the area, the

60-day exposure period, and the conditional core damage probability with the loss of the

Division I emergency diesel generator, the analyst calculated that the change in risk was

significantly less than 1E-6. Therefore, this finding was of very low safety significance

(Green).

- 37 -

Enclosure

A-1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

R. Benson, Manager (Acting), Radiation Protection

J. Browning, General Plant Manager

D. Coulter, Senior Licensing Specialist

H Farris, Assistant Operation Manager

K. Higgenbotham, Planning and Scheduling Manager

J. Houston, Maintenance Manager

R. Jackson, Licensing

C. Lewis, Manager, Emergency Preparedness

C. Perino, Licensing Manager

M. Perito, Site Vice President of Operations

M. Richey, Director, Nuclear Safety Assurance

F. Rosser, Supervisor, Dosimetry

R. Sumrall, Superintendant, Operations Training

R. Sylvan, Supervisor, Radiation Protection

T. Trichell, Radiation Protection Manager

D. Wiles, Engineering Director

R. Wilson, Manager, Quality Assurance

E. Wright, Supervisor, Radiation Protection

NRC Personnel

R. Smith, Senior Resident Inspector

A-2

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed 05000416/2011002-01 NCV Transient Combustible Stored in the Fire Exclusion Zone Near the

Independent Spent Fuel Storage Installation (Section 1R05)05000416/2011002-02 NCV Failure to Update Available Low Pressure Coolant Injection Loops

in the Updated Final Safety Analysis Report (Section 1R12)05000416/2011002-03 NCV Failure to Demonstrate Maintenance Effectiveness of Train B

Control Room Air Conditioner(Section 1R12)05000416/2011002-04 NCV

Failure to Use a Qualified Radiation Protection Technician to

Provide Direct Continuous Coverage of Work in a Locked High

Radiation Area (Section 2RS01)05000416/2011002-05 NCV Failure to Prevent Recurrence of Control Room Air Conditioner

Compressor Tripping Due to Low Oil Pressure (Section 4OA3)05000416/2011002-06 FIN

Inadequate Design Control for the Mitigation Monitoring System

Modification (Section 4OA3)

Closed

TI 2515/179

TI

Verification of Licensee Responses to NRC Requirement for

Inventories of Materials Tracked in the National Source Tracking

System Pursuant to Title 10, Code of Federal Regulations,

Part 20.2207 (10 CFR 20.2207) (Section 4OA5)

05000416/2010-002-00 LER Control Room Air Conditioning Inoperability - Loss of Both Trains

(Section 4OA3)

A-3

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1RO1: Adverse Weather Protection

PROCEDURE

NUMBER

TITLE

REVISION

ENS-EP-302

Severe Weather Response

11

05-1-02-VI-2

Hurricanes, Tornados, and Severe Weather

113

04-1-01-P41-1

Standby Service Water System

133

04-1-01-N71-1

Circulating Water System

72

04-1-03-A30-1

Cold Weather Protection

20

OTHER

NUMBER

TITLE

DATE

SSW Pump Discharge Temperatures

January 6-10,

2011

WORK ORDER

WO 52233022

Section 1RO4: Equipment Alignment

PROCEDURE

NUMBER

TITLE

REVISION

9.3-17 - 9.3-25

GG UFSAR

3

07-1-34-C41-

C001-1

Standby Liquid Control Pump

10

04-1-01-C41-1

Standby Liquid Control System

119

04-1-01-P75-1

Standby Diesel Generator System

88

04-1-01-P41-1

Standby Service Water System

133

04-1-01-E12-1

System Operating Instructions Residual Heat Removal

System

137

04-1-01-E12-1

Residual Heat Removal B

137

04-1-01-E12-1

Residual Heat Removal C

137

A-4

Attachment

PROCEDURE

NUMBER

TITLE

REVISION

04-1-01-E12-1

Residual Heat Removal B Attachment IB

137

04-1-01-E12-1

Residual Heat Removal B Attachment IIIB

137

04-1-01-E12-1

Residual Heat Removal C Attachment IC

137

04-1-01-E12-1

Residual Heat Removal B Attachment VB

137

04-1-01-E12-1

Residual Heat Removal (Interface Valves) Attachment IIE

137

04-1-01-P41-1

Standby Service Water System Attachment IIB

133

04-1-01-P41-1

Standby Service Water System Attachment IIIB

113

OTHER

NUMBER

TITLE

DATE

11-4568

Scaffolding Evaluation Request

February 15,

2001

CALCULATION

NUMBER

TITLE

DATE

9645

Diesel Generator Building Walls

August 2,

1976

C-C400

SSW CT and Basin (Pump-House) Tornado and No

Earthquake

May 28, 1976

C-0-100

Diesel Generator Bldg. Walls Tornado Wind Load W

August 2,

1976

WORK ORDER

WO 52256371

WO 00260559

WO 00259801

Section 1RO5: Fire Protection

PROCEDURE

NUMBER

TITLE

REVISION

Fire Pre-Plan DG-03 Division II Diesel Generator Room

3

9A-343 - 9A347

GG UFSAR

Fire Pre-Plan A-02

RHR A Pump Room 1A103

1

A-5

Attachment

PROCEDURE

NUMBER

TITLE

REVISION

Fire Pre-Plan A-03

RCIC Pump Room 1A104

1

Fire Pre-Plan A-04

RHR B Pump Room 1A105

1

9A.5.2.2

Safe Shutdown Equipment

Appendix 9B

Fire Protection Program

CONDITION REPORT

CR-GGN-2011-00862

CR-GGN-2011-01939

CR-GGN-2011-00851

CR-GGN-2011-00455

Section 1RO6: Flood Protection Measures

PROCEDURE

NUMBER

TITLE

REVISION /

DATE

9A-336 - 9A338

GG UFSAR

9A.5.59

GG UFSAR FIRE AREA 59

EN-OP-104

Operability Determination Process Immediate Determination

For Degraded of Nonconforming Conditions

4

OTHER

NUMBER

TITLE

DATE

Russell Daniel Oil Co. Inc. Delivery Date Schedule

February 10,

2011

CONDITION REPORT

CR-GGN-2011-00198

CR-GGN-2011-00562

CR-GGN-2011-00654

WORK ORDER

WO 52281566

WO 52210679 03

WO 52210679 02

WO 52210679 01

WO 00041743

WO 52210679

A-6

Attachment

ENGINEERING CHANGE

EC No. 24971

EC No. 24904

EC No. 24972

Section 1R07:

PROCEDURE

NUMBER

TITLE

REVISION

08-S-03-10

Chemistry Procedure-Closed Loops

48

OTHER

NUMBER

TITLE

DATE

CCE 2006-0002

Commitment Change Evaluation Form

Letter

Response to Generic Letter 89-13; Service Water System

Problems Affecting Safety-Related Equipment

January 29,

1990

WORK ORDER

WO 00178965 01

WO 00178965 02

WO 00178965 03

Section 1R11: Licensed Operator Requalification Program

OTHER

NUMBER

TITLE

REVISION /

DATE

GSMS-LOR-

WEX03

LOR Training-Double Recirculation Pump Trip/ATWS

January 18,

2011

Rev 17

Turnover and Simulator Differences 2011 Cycle 1 Simulator

Training

1

Per Control Room Walkdown, Modifications to TREX Load

January 7,

2011

Letter

Emergency Preparedness January 31, 2011 Simulator Drill

Performance Indicators

February 1,

2011

A-7

Attachment

Section 1R12: Maintenance Effectiveness

PROCEDURE

NUMBER

TITLE

REVISION /

DATE

EN-FP-S-001-

Multi

Engineering Standard-Appendix R Emergency Lighting Units

January 10,

2011

07-S-12-143

Big Beam Emergency Light Inspection, Battery Capacity

Verification, and Functional Test

2

EN-DC-203

Maintenance Rule Program

1

EN-DC-206

Maintenance Rule (a)(1) Process

1

EN-DC-207

Maintenance Rule Periodic Assessment

1

NMM EN-LI-118

Root Cause Evaluation Report Attachment IV (54 of 54)

12

EN-DC-205

Maintenance Rule Monitoring

2

GG UFSAR Table 7.5-1 Safety-Related Display

Instrumentation

GG UFSAR Table 7.5-2 Post-Accident Monitoring

Instrumentation

GG UFSAR 6.3 Emergency Core Cooling Systems

0

03-1-01-3

Integrated Operating Instructions Plant Shutdown

118

OTHER

NUMBER

TITLE

REVISION /

DATE

Emergency Lighting - GGNS Discussion of Recent Activities

Maintenance Rule Expert Panel June 22, 2010 Meeting

Minutes

Maintenance Rule Expert Panel August 10, 2010 Meeting

Minutes

Entergy Nuclear-GGNS Maintenance Rule Program Basis

Document, Control Room and Emergency Lighting (Z92)

System

0

Z92

Maintenance Rule Database Control Room and Emergency

Lighting

TM M348X.8001

Midtron 3200 Battery Conductance Tester

A-8

Attachment

OTHER

NUMBER

TITLE

REVISION /

DATE

VMA97/0181

Emergency Lights

Maintenance Rule Database Information - Main Control

Room Air Conditioning (Z51) System

March 21,

2009 to

December

23, 2010

Maintenance Rule Database Z51 Control Room HVAC

System

EC No.: 27856

Engineering Evaluation

0

Maintenance Rule Program (a)(1) Evaluation and Action Plan

Main Control Room Air Conditioning (Z51) System

Agenda for Maintenance Rule Expert Panel Meeting

February 4,

2010

RHR Heat Exchanger SSW Flow Indication (a)(1) Status

Maintenance Rule Database E12 RHR System

Maintenance Rule Program (a)(1) Evaluation for the Residual

Heat Removal (E12/RHR) System CR-GGN-2009-0754 CA

No. 002

Maintenance Rule (a)(1) Evaluation Standby Service Water

(P41) System (GR-GGN-2010-00305)

Agenda Items from Maintenance Rule Expert Panel Meeting

June 24,

2010

Agenda Items from Maintenance Rule Expert Panel Meeting

June 22,

2010

CONDITION REPORT

CR-GGN -2009-05330

CR-GGN -2010-00381

CR-GGN -2010-04575

CR-GGN -2010-04585

CR-GGN -2010-06346

CR-GGN -2011-00481

CR-GGN -2011-00521

CR-GGN -2011-01212

CR-GGN-2011-01650

CR-GGN-2010-01984

CR-GGN-2011-11505

CR-GGN-2011-01308

CR-GGN-2010-07315

CR-GGN-2009-00842

CR-GGN-2009-00754

GR-GGN-2009-01729

CR-GGN-2009-02477

CR-GGN-2009-03394

CR-GGN-2009-02947

CR-GGN-2009-02848

CR-GGN-2009-03292

CR-GGN-2009-03574

CR-GGN-2009-03592

CR-GGN-2009-04219

A-9

Attachment

CR-GGN-2010-01031

CR-GGN-2009-04048

CR-GGN-2009-05930

CR-GGN-2009-05215

CR-GGN-2009-05932

CR-GGN-2009-05472

CR-GGN-2009-06066

CR-GGN-2009-04733

CR-GGN-2010-00036

CR-GGN-2010-01329

CR-GGN-2011-00789

CR-GGN-2010-07351

CR-GGN-2010-04009

CR-GGN-2010-05892

CR-GGN-2011-00791

CR-GGN-2011-00820

CR-GGN-2011-00985

CR-GGN-2009-01204

CR-GGN-2010-00684

CR-GGN-2010-05290

CR-GGN-2010-01585

CR-GGN-2010-00800

CR-GGN-2010-01474

CR-GGN-2010-01337

CR-GGN-2009-05508

CR-GGN-2010-01320

CR-GGN-2010-01345

CR-GGN-2009-05731

CR-GGN-2009-06174

CR-GGN-2010-02797

CR-GGN-2010-02200

CR-GGN-2010-03655

CR-GGN-2010-04629

CR-GGN-2010-02990

CR-GGN-2010-03241

CR-GGN-2009-00350

CR-GGN-2009-00426

CR-GGN-2009-00846

CR-GGN-2009-01518

CR-GGN-2010-02805

CR-GGN-2010-04015

CR-GGN-2010-03333

CR-GGN-2010-04625

CR-GGN-2010-04255

CR-GGN-2009-05527

CR-GGN-2010-02974

CR-GGN-2010-06137

CR-GGN-2010-05208

CR-GGN-2010-05330

CR-GGN-2010-04686

CR-GGN-2010-04963

CR-GGN-2010-05572

CR-GGN-2010-03650

CR-GGN-2010-06978

CR-GGN-2010-06148

CR-GGN-2010-06150

CR-GGN-2010-05328

CR-GGN-2010-06142

CR-GGN-2011-00403

CR-GGN-2011-00749

CR-GGN-2011-00819

CR-GGN-2011-00850

CR-GGN-2010-06895

CR-GGN-2010-06918

CR-GGN-2011-01212

CR-GGN-2010-05147

WORK ORDER

WO 52255810

WO 52223396

WO 52271013 01

WO 52196016

WO 52220690

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

PROCEDURE

NUMBER

TITLE

REVISION

EN-WM-101

On-line Work Management Process

7

EN-WM-100

Work Request Generation, Screening and Classification

5

EN-WM-101

On-line Work Management Process

8

EN-WM-101

On Line Emergent Work Addition/Deletion Approval Form for

the Week of March 7, 2011

7

A-10

Attachment

PROCEDURE

NUMBER

TITLE

REVISION

EN-WM-101

On Line Emergent Work Addition/Deletion Approval Form for

the Week of February 28, 2011

7

WORK ORDER

WO250074

WO247598

WO52290243

WO52290462

WO52290463

WO52290464

WO70346

WO52291451

WO52291458

WO52291454

WO52291456

WO52291689

WO52291690

WO261213

WO52284287

WO52269835

WO52290236

WO52290463

WO52290464

WO52291844

WO52291454

WO52291456

WO261601

WO250966-02

WO237429

WO256910-01

WO52290639

WO52287735

WO52290638

WO52287736

WO52276935

WO260417

WO260212-02

WO260212-01

WO00219198

WO260529-07

WO52204865

WO260503

WO52243284

WO260529-07

WO52204865

WO52199495

WO255787-01,02,03,04

WO52249417

WO52271012

WO261175

WO259639

WO257881

WO200935-02

WO00257063

WO224859

WO261706

WO255360-08

WO263130

WO261181-01 and 02

WO262143

WO234988-04

WO234992-04

WO52250110-03

WO234985-04

WO259003-05

WO259005-05

WO259007-05

WO112951-08

WO52270042

WO52259286

WO52275616

WO52288663

WO52290468

WO52270252

WO52291424

WO52270250

WO52291423

WO235034

WO52288844

WO51563342

WO160041

WO52290473

WO52281103

A-11

Attachment

Section 1R15: Operability Evaluations

PROCEDURE

NUMBER

TITLE

REVISION

EN-OP-104

Operability Determination Process

4

EN-DC-115

EC No. 20228

0

CALCULATION

NUMBER

TITLE

REVISION

PDS0170B

SSW Basin A Relief Valve

2

DRAWING

NUMBER

TITLE

REVISION

FSK-M-KC187-

01C1-Y

Design Change Drawing SSW Basin A and B

8

Design Change Drawing Reinforced Concrete Distribution

Support System Tower Elevation 157-8

8

OTHER

NUMBER

TITLE

REVISION /

DATE

2007-029

LBDCR Initiation

Grand Gulf Nuclear Station, Unity 1 - Conforming License

Amendment to Incorporate the Mitigation Strategies Required

by Section B.5.b of the Commission Order EA - 02 - 026

July 18, 2007

GNRO-

2007/00037

Supplementary Response Regarding Implementation Details

for the Phase 2 and 3 Mitigation Strategies Grand Gulf

Nuclear Station

June 7, 2007

NEI 06-12

B.5.b Phase 2 & 3 Submittal Guideline

Rev 2

December

2006

7-15

GG FSAR

Rev 59

9.5-3

GG UFSAR

Attachment 9.2

Immediate Determination for Degraded of Nonconforming

Conditions CR-GGN-2011-01512

A-12

Attachment

OTHER

NUMBER

TITLE

REVISION /

DATE

Attachment 9.5

Operability Evaluation CR-GGN-2011-00155

NUS Switch Status

CONDITION REPORT

CR-GGN-2011-01173

CR-GGN-2011-00765

CR-GGN-2011-00155

CR-GGN-2011-00766

CR-GGN-2011-00799

CR-GGN-2011-01512

CR-GGN-2009-06838

CR-GGN-2011-01349

CR-GGN-2011-04701

CR-GGN-2011-00369

CR-GGN-2011-00643

CR-GGN-2011-00647

CR-GGN-2011-00665

CR-GGN-2011-00666

CR-GGN-2011-00667

CR-GGN-2011-00668

CR-GGN-2011-00669

CR-GGN-2011-00670

CR-GGN-2011-00671

Section 1R18: Plant Modifications

PROCEDURE

NUMBER

TITLE

REVISION

EN-DC-136

Temporary Modifications

5

EN-LI-102

Corrective Action Process

16

DRAWING

NUMBER

TITLE

REVISION

E-1187-007

E31 Leak Detection System RWCU Flow Circuit Computer

Input

7

E1165014

Schematic Design Rod Control and Information System Rod

Position Information and SCRAM Time Test

13

E1173028

Schematic Design Reactor Protection System Testability

6

M1051A

Main and Reheat System

33

OTHER

NUMBER

TITLE

06-OP-1000-D-0001 Log Data

A-13

Attachment

OTHER

NUMBER

TITLE

CR-GGN-2009-

02198 CA 26

CR Periodic Review (initial at 6 months/follow by annual)

and/or Long Tem CA Classification Form

CONDITION REPORT

CR-GGN-2009-02198

CR-GGN-2010-04451

CR-GGN-2011-01231

WORK ORDER

WO00238932

WO00238928

WO00193921

WO00193920

WO002239736-01

WO002239736-02

WO002239736-03

ENGINEERING CHANGE

EC22768

EC22625

EC22635

Section 1R19: Postmaintenance Testing

PROCEDURE

NUMBER

TITLE

REVISION /

DATE

06-OP-1E12-Q-

0005

LPCI/RHR Subsystem A MOV Functional Test

112

06-OP-1E12-Q-

0023

LPCI/RHR Subsystem A Quarterly Functional Test

121

06-0P-1E12-

0006

LPCI/RHR System B MOV Functional Test

111

06-OP-1P41-Q-

0004

Standby Service Water Loop A Valve AND Pump Operability

Test

119

04-1-03-P75-1

Div 1 Diesel Generator Unexcited Run

7

06-OP-1P75-M-

001

Data Sheet III Standby Diesel Generator 11 Functional Test

February 12,

2011

07-S-12-40

General Cleaning and Inspection of Rotating Electrical

Equipment

2

07-S-12-146

General Maintenance Instruction Motor Off Line Diagnostic

1

A-14

Attachment

PROCEDURE

NUMBER

TITLE

REVISION /

DATE

Data Acquisition

07-S-12-55

Insulation Resistance Testing

10

06-IC-1E22-Q-

0004

HPCS System Flow Rate - Low (Bypass) Functional Test

104

OTHER

NUMBER

TITLE

DATE

RPS Motor GEN B - MCE Stator

February 2,

2011

HPCS Min Flow Valve Position

March 18,

2011

DRAWING

NUMBER

TITLE

DATE

BRKR No. 52-

142229

IC71SOOIOB

BRKR No. 52-

142229

IC7IS003B (Local C71-S003B)

BRKR No. 52-

142229

IC7IS003D (Local C71-S003D)

Timeline for Events leading to NRC Notification Call on

HPCS

March 18,

2011

CONDITION REPORT

CR-GGN-2011-00945

WORK ORDER

WO52311451

WO52311569

WO52285575

WO00251847

WO52224645

WO52223715

WO00262318

WO00259110-01

WO00259110-03

WO00237650-01

WO00237650-04

WO00237650-05

WO00237650-06

WO52304041

WO00270205-01

A-15

Attachment

WO00270205-02

Section 1R22: Surveillance Testing

PROCEDURE

NUMBER

TITLE

REVISION

06-CH-1B21-O-

0002

Reactor Coolant Routine Chemistry-Sample February 23,

2011

106

06-CH-1B21-O-

0002

Reactor Coolant Routine Chemistry-Sample February 18,

2011

106

06-CH-1B21-O-

0002

Plant Operations Manual-Reactor Coolant Routine Chemistry

106

06-CH-1B21-W-

0008

Reactor Coolant Dose Equivalent Iodine

104

06-OP-1C61-R-

0002

Functional Checks with E51 Valves

109

06-OP-1P75-M-

0001

Standby Diesel Generator Functional Test

132

06-IC-1D17-R-

0010

Fuel Handling Area Ventilation Exhaust High High Radiation

Electronics Time Response Test

102

04-1-01-P81-1

High Pressure Core Spray Diesel Generator

67

06-OP-1P81-M-

0002

HPCS Diesel Generator 13 Functional Test

123

EN-OP-109

Conduct of Operations

2

OTHER

NUMBER

TITLE

DATE

Drywell Unidentified Leakage Rate vs. A Recirc Seal Delta

T

June 2010-

January 2011

CONDITION REPORT

CR-GGN-2011-01932

CR-GGN-2011-01868

WORK ORDER

WO52271012

WO52289870

WO52288401

WO52261837

WO52307262

WO00270146-01

A-16

Attachment

Section 1EP6: Drill Evaluation

OTHER

NUMBER

TITLE

DATE

Emergency Facility Log

March 3, 2011

Repair and Corrective Action Table

March 3, 2011

Emergency Notification Form 1-7 for EP Drill

March 3, 2011

GGNS 2011 1st Quarter ERO Training Drill

CONDITION REPORT

CR-GGN-2011-01481

CR-GGN-2011-01486

CR-GGN-2011-01495

CR-GGN-2011-01499

CR-GGN-2011-01510

CR-GGN-2011-01519

CR-GGN-2011-01520

CR-GGN-2011-01522

Section 2RS01: Radiological Hazard Assessment and Exposure Controls

PROCEDURES

NUMBER

TITLE

REVISION

EN-RP-100

Radiation Worker Expectations

6

EN-RP-101

Access Control for Radiologically Controlled Areas

5

EN-RP-102

Radiological Control

2

EN-RP-106

Radiological Survey Documentation

2

01-S-08-1

Administration of the GGNS Radiation Protection Program

105

01-S-08-6

Radioactive Source Control

113

08-S-02-50

Radiological Surveys and Surveillances

116

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

NUMBER

TITLE

DATE

LO-GLO-2010-93

Pre-NRC Rad Hazard Assessment and Exposure

Controls Assessment

December 16, 2010

CONDITION REPORTS

CR-GGN-2011-00183 CR-GGN-2011-00551 CR-GGN-2011-00655 CR-GGN-2011-00926

CR-GGN-2011-00740

A-17

Attachment

RADIOLOGICAL SURVEY

NUMBER

TITLE

DATE

GG-1102-0146

Routine Daily Surveys

February 15, 2011

GG-1012-0083

208 CTMT Entire Elevation

December 7, 2010

GG-1102-0152

208 CTMT Entire Elevation

February 15, 2011

GG-1012-0118

119 AB RHR A Room

December 9, 2010

GG-1012-0086

119 AB RHR A Room

February 7, 2011

GG-1011-0254

119 AB RHR B Room

November 30, 2010

GG-1101-0156

119 AB RHR B Room

January 16, 2011

GG-1011-0064

93 Aux RHR C & ADHR Hx Rooms

November 6, 2010

GG-1102-0044

93 Aux RHR C & ADHR Hx Rooms

February 3, 2011

GG-1011-0018

119 Aux Piping Penetration & Valve Room

November 2, 2010

GG-1102-0041

119 Aux Piping Penetration & Valve Room

February 3, 2011

GG-1011-0063

93 Aux HPCS Pump Room

November 6, 2010

GG-1102-0042

93 Aux HPCS Pump Room

February 3, 2011

RADIATION WORK PERMITS

NUMBER

TITLE

20101005

Tours and Inspections into all areas

20111054

Locked High Radiation Area Entries for Plant/System Investigations, Valve

Manipulations, Tagouts, and Misc. Activities

20111058

Maintenance in HRA /HCA & Above

Section 2RS02: Occupational ALARA Planning and Controls

PROCEDURES

NUMBER

TITLE

REVISION

EN-RP-105

Radiological Work Permits

9

EN-RP-110

ALARA Program

7

AUDITS, SELF-ASSESSMENTS, AND SURVEILLANCES

NUMBER

TITLE

DATE

LO # LO-GLO-

2010-00094

Pre-NRC Inspection for ALARA Planning and Controls-

Assessment

November 9, 2010

CONDITION REPORTS

A-18

Attachment

CR-GGN-2011-00425 CR-GGN-2011-00425 CR-GGN-2010-06335

RADIATION WORK PERMIT PACKAGES

NUMBER

TITLE

2010-1402

Refuel Floor High Water Activities

2010-1403

Reactor Disassemble/Reassemble

2010-1508

Under Vessel Activities

2010-1530

B Recirc Pump Replacement

2010-1534

B21F011B Stem Replacement

Section 4OA1: Performance Indicator Verification

PROCEDURE

NUMBER

TITLE

REVISION

EN-LI-114

1st Quarter 2010 Unplanned Scrams per 7,000 Critical

Hours

4

EN-LI-114

2nd Quarter 2010 Unplanned Scrams per 7,000 Critical

Hours

4

EN-LI-114

3rd Quarter 2010 Unplanned Scrams per 7,000 Critical

Hours

4

EN-LI-114

4th Quarter 2010 Unplanned Scrams per 7,000 Critical

Hours

4

EN-LI-114

1st Quarter 2010 Unplanned Scrams with Complications

4

EN-LI-114

2nd Quarter 2010 Unplanned Scrams with Complications

4

EN-LI-114

3rd Quarter 2010 Unplanned Scrams with Complications

4

EN-LI-114

4th Quarter 2010 Unplanned Scrams with Complications

4

EN-LI-114

1st Quarter 2010 Unplanned Power Changes per 7,000

Critical Hours

4

EN-LI-114

2nd Quarter 2010 Unplanned Power Changes per 7,000

Critical Hours

4

EN-LI-114

3rd Quarter 2010 Unplanned Power Changes per 7,000

Critical Hours

4

EN-LI-114

4th Quarter 2010 Unplanned Power Changes per 7,000

Critical Hours

4

A-19

Attachment

OTHER

NUMBER

TITLE

January 2010 Core Thermal Power

February 2010 Core Thermal Power

March 2010 Core Thermal Power

April 2010 Core Thermal Power

May 2010 Core Thermal Power

June 2010 Core Thermal Power

July 2010 Core Thermal Power

August 2010 Core Thermal Power

September 2010 Core Thermal Power

October 2010 Core Thermal Power

November 2010 Core Thermal Power

December 2010 Core Thermal Power

Section 4OA2: Identification and Resolution of Problems

OTHER

NUMBER

TITLE

DATE

GGNS Position on Riley Temperature Switch Replacement

Maintenance Rule Program Functional Failures-Riley

Temperature Switches

NUS Switch Status

February 2,

2011

Riley History Discussion by Lee Eaton

Riley History Presentation to 2009 PInR

CONDITION REPORT

CR-GGN-2009-05879

A-20

Attachment

Section 4OA3: Event Follow-Up

PROCEDURE

NUMBER

TITLE

REVISION

EN-DC-167

Classification of Structures, Systems, and Components

3

EN-HU-103

Human Performance Error Reviews for CR-GGN-2010-7877

4

EN-DC-115

Engineering Change Process

11

DRAWINGS

NUMBER

TITLE

REVISION

M-1127A

Piping and Instrumentation Diagram Noblechem Monitoring

System

0

M-1081B

Control Rod Drive Hydraulic System

28

M-1078A

Reactor Recirculation System Unit 1

33

M-1079

Reactor Water Clean-up System Unit 1

46

M-1069A

Process Sampling System Unit 1

24

OTHER

NUMBER

TITLE

DATE

Root Cause Evaluation Report-Control Room Air Conditioner

B Trip (Event Date 10-14-2010)

October 16,

2010

GNRO-

2010/00077

LER 2010-002-00Control Room Air Conditioning

December

13, 2010

Root Cause Evaluation Report Mitigation Monitor Durability

Monitor Pump Failure

November 8,

2010

MMS Skid Piping/Component Design Basis

Compliance with NRC Regulatory Guide 1.26

CONDITION REPORT

CR-GGN-2010-07315

CR-GGN-2010-08580

CR-GGN-2010-07852

ENGINEERING CHANGE

A-21

Attachment

EC13135

EC13132

EC13138

Section 4OA5 Temporary Instruction 2515/179

PROCEDURES

NUMBER

TITLE

REVISION

EN-RP-143

Source Control

7

MISCELLANEOUS DOCUMENTS

TITLE

DATE

National Source Tracking System Annual Inventory Reconciliation Report

2010

National Source Tracking System Annual Inventory Reconciliation Report

2011

Section 4OA7: Licensee-Identified Violations

CONDITION REPORT

CR-GGN-2011-00851