IR 05000271/2006003: Difference between revisions

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| issue date = 07/27/2006
| issue date = 07/27/2006
| title = IR 05000271-06-003, on April 1, 2006 Through June 30, 2006, Vermont Yankee Nuclear Power Station
| title = IR 05000271-06-003, on April 1, 2006 Through June 30, 2006, Vermont Yankee Nuclear Power Station
| author name = Powell R J
| author name = Powell R
| author affiliation = NRC/RGN-I/DRP/PB5
| author affiliation = NRC/RGN-I/DRP/PB5
| addressee name = Sullivan T A
| addressee name = Sullivan T
| addressee affiliation = Entergy Nuclear Operations, Inc
| addressee affiliation = Entergy Nuclear Operations, Inc
| docket = 05000271
| docket = 05000271
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=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:EnclosureJuly 26, 2006Mr. Theodore A. SullivanSite Vice President Entergy Nuclear Operations, Inc.
[[Issue date::EnclosureJuly 26, 2006]]


Mr. Theodore A. SullivanSite Vice President Entergy Nuclear Operations, Inc.
Vermont Yankee Nuclear Power Station 320 Governor Hunt Road Vernon, VT 05354SUBJECT:VERMONT YANKEE NUCLEAR POWER STATION - NRC INTEGRATEDINSPECTION REPORT 05000271/2006003
 
Vermont Yankee Nuclear Power Station 320 Governor Hunt Road Vernon, VT 05354
 
SUBJECT: VERMONT YANKEE NUCLEAR POWER STATION - NRC INTEGRATEDINSPECTION REPORT 05000271/2006003


==Dear Mr. Sullivan:==
==Dear Mr. Sullivan:==
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In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/Raymond J. Powell, ChiefProjects Branch 5 Division of Reactor Projects Enclosure 2cc w/encl:M. R. Kansler, President, Entergy Nuclear Operations, Inc.
Sincerely,
/RA/Raymond J. Powell, ChiefProjects Branch 5 Division of Reactor Projects Enclosure 2cc w/encl:M. R. Kansler, President, Entergy Nuclear Operations, Inc.


G. J. Taylor, Chief Executive Officer, Entergy Operations J. T. Herron, Senior Vice President and Chief Operating Officer C. Schwarz, Vice-President, Operations Support O. Limpias, Vice President, Engineering J. M. DeVincentis, Manager, Licensing, Vermont Yankee Nuclear Power Station Operating Experience Coordinator, Vermont Yankee Nuclear Power Station W. Maguire, General Manager, Plant Operations, Entergy Nuclear Operations, Inc.
G. J. Taylor, Chief Executive Officer, Entergy Operations J. T. Herron, Senior Vice President and Chief Operating Officer C. Schwarz, Vice-President, Operations Support O. Limpias, Vice President, Engineering J. M. DeVincentis, Manager, Licensing, Vermont Yankee Nuclear Power Station Operating Experience Coordinator, Vermont Yankee Nuclear Power Station W. Maguire, General Manager, Plant Operations, Entergy Nuclear Operations, Inc.
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===Closed===
===Closed===
: 05000271/2004007-01VIODid Not Keep Adequate Records, Follow Procedures, andPerform Physical Inventory of Special Nuclear Material
05000271/2004007-01VIODid Not Keep Adequate Records, Follow Procedures, andPerform Physical Inventory of Special Nuclear Material
(Section 4OA2.3)
(Section 4OA2.3)05000271/2005005-03URIInformation Needed to Validate the Direct DoseCalculation Method in ODCM Section 6.11.1  
: [[Closes finding::05000271/FIN-2005005-03]]URIInformation Needed to Validate the Direct DoseCalculation Method in ODCM Section 6.11.1  
(Section 2PS3)05000271/2006002-01URITraining Provided to Licensed Operators Regarding PlantResponse to a Condensate Pump Trip (Section 4OA5.2)
(Section 2PS3)
: [[Closes finding::05000271/FIN-2006002-01]]URITraining Provided to Licensed Operators Regarding PlantResponse to a Condensate Pump Trip (Section 4OA5.2)
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 2PS3: Radiological Environmental Monitoring Program ProceduresOP 4505Source Calibration of Main Steam Line Radiation MonitorsOP 4658Periodic Evaluation of Direct Dose From Plant Operation==
==Section 2PS3: ==
: A-2AttachmentMiscellaneous DocumentsGE-Reuter Stokes User's Manual for Pressurized Ion ChamberSection 4OA2.1:
: Radiological Environmental Monitoring Program ProceduresOP 4505Source Calibration of Main Steam Line Radiation MonitorsOP 4658Periodic Evaluation of Direct Dose From Plant Operation
: Routine Review of Identification and Resolution of Problems Condition Reports2004-1474"A" SW discharge valve bonnet guide ribs severely worn2005-3633A EDG potential transformer fuse blown annunciator momentarily received
: 2006-0950 Unanticipated dose rate alarm during dose rate verification survey
: 2006-0958 Four strain gages installed as part of the Steam Dryer monitoring plan for EPUappear to be providing inaccurate readings2006-0960Ground water leak on torus floor
: 2006-0961Eight accelerometers installed as part of the piping vibration monitoring planappear to be non-functioning2006-0962Observation of increased vibration of conduit associated with LSH-101-38A
: 2006-0966The difference between steam flow and feed flow is increasing as reactor poweris raised to 100% EPU2006-0986Recombiner "A" failed to warm up after attempted repair of MS-107-1A
: 2006-1018Steam Dryer level 2 performance criteria exceeded during power ascension
: 2006-1031Condensate demineralizer inadvertently removed from service when wrong valvewas manipulated2006-1038EQ qualified life relay replacements not performed for assets 5-12C(X) & 5-12D(X)2006-1083Siren controller radio was found unplugged at the Bernardston Fire Station
: 2006-1134 Breaker opened inadvertently while operator was hanging tags
: 2006-1137 Cross-contamination (non-rad dye) of potable water system when a contractor
: 2006-1164Excessive black exhaust exiting EDG stack during surveillance run on April 20,2006 is in violation of State of VT regulations2006-1197Steam/Feed mismatch observed
: 2006-1210During the performance of
: ERSTI-04-VY1-1409-000, Level 2 acceptance criteriafor Total Steam flow deadband was exceeded2006-1249Main steam line pressure drop larger than expected at 1832 MWth
: 2006-1260Moisture carryover analysis result >0.10% after power increase to 1872 MWth
: 2006-1360Moisture carryover analysis result >0.10% at 1912MWth
: 2006-1404Unable to close SW pump discharge valve SW-2D
: 2006-1406D SW pump discharge valve will not fully close
: 2006-1413The D SW LCO was not able to commence due to the inability to close V70-2D
: 2006-1427'A' RHR heat exchanger cleaning period exceeds 18 month requirement
: 2006-1446 Fuel pooling cooling pump tripped due to operator starting the pump without asuction path established2006-1470Less than minimum staffing 5/15/06 2346
: 2006-1570*NRC identified that I&C personnel took as-left voltage readings from incorrectRPIS power supply2006-1583Fire damper not closing consistently
: A-3Attachment2006-1593Diesel Generator day tank high and low alarm switches not checked monthly asper TS bases 4.10.A2006-1641HPCI-14 cycling after HPCI freedom of movement test
: 2006-1660The 5/24/06 ground fault on Bus 2 resulted in East switchgear CO2 initiation andunusual event declaration2006-1737Expected site boundary exposure rates are higher than postulated in calculationsprepared prior to plant power uprate2006-1738Installation of HP Turbine Shield impacts the Offsite Dose Calculation Manualmethod for determining the maximum contribution of direct dose due to Nitrogen-
: 2006-1740 SM authorized tag removal from RHRSW pump without considering impact onoperability of core spray pump in same room2006-1805 Improper weapon manipulation in armory
: 2006-2037Following the "A" EDG 2 hour load test, the #60 relay Line B LOW target was in
: 2006-2046*An existing workaround was not contained in pre-job briefing form for EDG faststart test.
: It was in slow start form.* Inspector-identified issues.Section 4OA2.2:
: Semi-Annual Trend ReviewProceduresEN-LI-102Corrective Action ProcessEN-LI-121 Entergy Trending ProcessCondition Reports2006-0967 RP tech performing survey became contaminated2006-0973 RP tech errors when ED alarmed
: 2006-0974 Failure to document radiological conditions briefing
: 2006-1110 Multiple entries made under high rad RWP without documented rad briefing
: 2006-1148 Sealand container missing required lock
: 2006-1031 Condensate demineralizer inadvertently removed from service when wrong valvewas manipulated2006-1134 Breaker opened inadvertently while operator was hanging tags
: 2006-1137 Cross-contamination (non-rad dye) of potable water system when a contractorconnected unauthorized equipment to the potable water supply to clean cooling towers2006-1314 Emerging trend in RP department HU error precursors
: 2006-1446 Fuel pool cooling pump tripped due to operator starting the pump without asuction path established2006-1492 Operations department HU performance indicator is red
: 2006-1570 NRC identified that I&C personnel took as-left voltage reading from incorrectRPIS power supply2006-1740 SM authorized tag removal from RHRSW pump without considering impact onoperability of core spray pump in same room
: A-4Attachment2006-1805 Improper weapon manipulation in armoryMiscellaneous Documents/ReportsVermont Yankee Quarterly Trend Report, First Quarter 2006Vermont Yankee Human Performance PIs for the station, the operations department, and the radiological protection departmentSection 4OA2.3:
: Annual Sample Review - Special Nuclear Material ControlsProceduresEN-NF-200Special Nuclear Material Control, Rev. 1, dated 12/4/2005EN-NF-202Tamper Proof Seals for Special Nuclear Material, Rev. 1, dated 12/4/2005
: EN-NF-104Special Nuclear Materials Program, Rev. 1, dated 12/4/2005Condition Reports and Work Tasks2004-1339Two fuel rod pieces not properly tracked2004-1906Process for tamper-evident devices not fully effective to ensure accounting of
: SNM2004-2562Physical inspection of SFP failed to identify SNM container
: 2004-3837SNM tamper-evident seal on gang box found broken during annual physicalinventory of onsite SNM2005-3159Box containing SNM with tamper seal opened prior to notifying ReactorEngineering2005-3993CR 2005-3159 identified corrective actions, but did not generate CAs
: 2006-0022CR 2004-1339 was closed without completion of recommended correctiveactionsLO 2004-0346Perform bench-marking in the area of Reactor EngineeringLO 2004-0329Followup verification for CR 2004-1339
: LO 2004-0492Perform snap-shot self-assessment of SNM during refueling
: LO 2004-0494Perform management observation of annual SNM inventory
: LO 2005-0206Training for new Entergy fleet SNM proceduresWT 2005-0000,
: CA 00417Forward SNM case study to managers and supervisors forpresentation at monthly staff meetingsWT 2005-0000,
: CA 00992Establish a standard for signs and postings
: WT 2005-0000,
: CA 00998Review signs and postings against new standard
: WT 2005-0000,
: CA 01948Review
: CR 2004-1339, CA 9 and
: CA 20 to ensure actions are completeWT 2005-0000,
: CA 01976Consider including SNM program requirements in pre-outage orannual refresher training for general staff
: A-5AttachmentAssessment ReportsCARB Effectiveness Review Report "Results of Effectiveness Review for
: CR-VTY-2004-1339, "The Loss of Accountability of SNM,"" dated 6/13/2005QA Surveillance Report
: QS-2005-VY-028, "SNM Controls Assessment," dated 1/4/2006
: VY Benchmark Report "SNM Control and Process," dated 1/20/2005
: VY Snapshot Self-Assessment Report, "Special Nuclear Materials Self-Assessment for RFO25 Activities and SNM Inventory 2005," dated 1/18/2006Section 4OA2.4:
: Annual Sample:
: Failure of Emergency Diesel Generator Loss of FieldRelaysProceduresOP 4126Diesel Generator SurveillanceDrawings5920-3909 Emergency Diesel Generator AC Schematic Diagram, Rev. 115920-3910 Emergency Diesel Generator DC Schematic Diagram, Rev. 15
: 20-3992 Emergency Diesel Generator Engine Control, Rev. 9
: 20-4152Emergency Diesel Generator Interconnection Diagram - Static Exciter, Rev. 1
: B-191301Sh.327A, "4KV Swgr #3, Compt 9, 4KV Swgr #3 Tie to 4KV Swgr #1 Bkr #3T1",Rev. 0B-191301Sh.328A, "4KV Swgr. #3, Compt. 10, Diesel Generator
: DG1-1B Bkr. & Lnp.Ckt.", Rev. 11MiscellaneousER 05-0992, Emergency Diesel Generator KLF Loss of Field Relay Modification - NuclearChange, Minor Calculation Change Document under
: ER-05-0992 for Calculation VYC-1671,
: EDG A & B Protective Relay Settings Verification Vermont Yankee Night Orders Book Vermont Yankee Pre-Job Briefs for the Diesel Generator Monthly Start and Load Tests Licensed Operator Requalification Training Program,
: LOR-25-205
: ResponsesWestinghouse Infogram IG93010, GVER-93-202
: Work Order 05-04242-000
: Work Order 05-04242-001
: A-6AttachmentCondition Reports2005-3622Loss of "B" EDG during ECCS test on 11/06/20052005-3633DG-1-1A potential transformer fuse blown annunciator momentarily receivedduring ECCS integrated test following the start of the
: RFO 25 ECCS integrated test2005-3854The
: EDG-1-1A and
: DG-1-1B loss of field relays may not adequately protect theEDGs during a loss of field event when operating in parallel with the Grid2005-3979The impedance unit which is internal to the
: DG-1-1B loss of field relay was foundto be in the actuated position2005-3981The trip setting of "A" and "B" diesel generator loss of field impedance units areset closer to the operating point of the EDG than desired 2006-1112EDG-some delay in sending 30 year old relay to lab for failure analysis per CA
: 2006-1433* Editorial error describing KLF loss of field relay target tap setting in VYC-1671
: 2006-1438*Administrative issue identified with the tracking of the diesel generator loss offield relays* Inspector-identified Issues.Section 4OA3.1:
: Indications of a Fire in the East Switchgear Room and the Declarationof an Unusual EventProceduresEAL U-4-a Any Unplanned On-Site or In-Plant Fire Not Extinguished Within 10 MinutesOP 0105Reactor Operations
: OP 3020 Fire Emergency Response Procedure
: OP 3540 Control Room Actions During an EmergencyCondition Reports2006-1574 Ground on bus 22006-1660 The 5/24/06 ground fault on bus 2 resulted in East switchgear CO2 initiation andUnusual Event declarationMiscellaneous DocumentsControl Room LogsSection 4OA5.4:
: NRC Temporary Instruction (TI) 2515/165, "Operational Readiness ofOffsite Power and Impact on Plant Risk
"ProceduresAP-0172Work Schedule Risk Management-Online, Rev 7
: ENN-PL-158Transmission Grid Interface, Rev 0
: ON 3179Grid Instability, Rev 0 
: A-7AttachmentOP
: 2140345 KV Electrical System, Rev 27
==LIST OF ACRONYMS==
ADAMSAgencywide Documents Access and Management SystemANSI/ANSAmerican National Standards Institute/American Nuclear Society
CFRCode of Federal Regulations
CO2Carbon Dioxide
CRCondition Report
DPVermont Yankee Department Procedure
EALEmergency Action Level
EDGEmergency Diesel Generator
EPAEnvironmental Protection Agency
EPUExtended Power Uprate
EREngineering Request
ERSTIEngineering Request Special Test Instruction
FAFire Area
FZFire Zone
HPCIHigh Pressure Coolant Injection
IPEEEIndividual Plant Examination External Events
INPOInstitute of Nuclear Power Operations
IRInspection Report
MHCMechanical Hydraulic Control
MSIVMain Steam Isolation Valve
MWthThermal Megawatts
NEINuclear Energy Institute
NRCNuclear Regulatory Commission
NRRNuclear Reactor Regulation
ODCMOffsite Dose Calculation Manual
OEOperating Experience
OPVermont Yankee Operating Procedure
PARSPublicly Available Records
PCISPrimary Containment Isolation System
PIPerformance Indicator
PMTPost Maintenance Testing
QAQuality Assurance
REMPRadiological Environmental Monitoring Program
RFORefueling Outage
RHRResidual Heat Removal
RHRSWResidual Heat Removal Service Water
RPRadiation Protection
RPSReactor Protection System
RPISRod Position Indicating System
SNMSpecial Nuclear Material
SWService Water
TATemporary Alteration
A-8AttachmentTITest Inspection TSTechnical Specification
UEUnusual Event
UFSARUpdated Final Safety Analysis Report
URIUnresolved Item
VIOViolation
VYVermont Yankee
WANOWorld Association of Nuclear Operators
: [[WOW]] [[ork Order]]
}}
}}

Revision as of 14:27, 13 July 2019

IR 05000271-06-003, on April 1, 2006 Through June 30, 2006, Vermont Yankee Nuclear Power Station
ML062080415
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 07/27/2006
From: Racquel Powell
NRC/RGN-I/DRP/PB5
To: Ted Sullivan
Entergy Nuclear Operations
References
IR-06-003
Download: ML062080415 (31)


Text

EnclosureJuly 26, 2006Mr. Theodore A. SullivanSite Vice President Entergy Nuclear Operations, Inc.

Vermont Yankee Nuclear Power Station 320 Governor Hunt Road Vernon, VT 05354SUBJECT:VERMONT YANKEE NUCLEAR POWER STATION - NRC INTEGRATEDINSPECTION REPORT 05000271/2006003

Dear Mr. Sullivan:

On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection atyour Vermont Yankee Nuclear Power Station. The enclosed report documents the inspectionfindings which were discussed on July 12, 2006, with members of your staff.The inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.Based on the results of this inspection, no findings of significance were identified.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/Raymond J. Powell, ChiefProjects Branch 5 Division of Reactor Projects Enclosure 2cc w/encl:M. R. Kansler, President, Entergy Nuclear Operations, Inc.

G. J. Taylor, Chief Executive Officer, Entergy Operations J. T. Herron, Senior Vice President and Chief Operating Officer C. Schwarz, Vice-President, Operations Support O. Limpias, Vice President, Engineering J. M. DeVincentis, Manager, Licensing, Vermont Yankee Nuclear Power Station Operating Experience Coordinator, Vermont Yankee Nuclear Power Station W. Maguire, General Manager, Plant Operations, Entergy Nuclear Operations, Inc.

N. Rademacher, Director NSA, Vermont Yankee Nuclear Power Station J. F. McCann, Director, Licensing C. D. Faison, Manager, Licensing M. J. Colomb, Director of Oversight, Entergy Nuclear Operations, Inc.

T. C. McCullough, Assistant General Counsel, Entergy Nuclear Operations, Inc.

J. H. Sniezek, PWR SRC Consultant M. D. Lyster, PWR SRC Consultant S. Lousteau, Treasury Department, Entergy Services, Inc.

Administrator, Bureau of Radiological Health, State of New Hampshire Chief, Safety Unit, Office of the Attorney General, Commonwealth of Mass.

J. E. Silberg, Pillsbury, Winthrop, Shaw, Pittman LLP G. D. Bisbee, Esquire, Deputy Attorney General, Environmental Protection Bureau J. Block, Esquire J. P. Matteau, Executive Director, Windham Regional Commission D. Katz, Citizens Awareness Network (CAN)

R. Shadis, New England Coalition Staff G. Sachs, President/Staff Person, c/o Stopthesale C. McCombs, Director, Commonwealth of Massachusetts, SLO Designee State of New Hampshire, SLO Designee State of Vermont, SLO Designee Enclosure 3Distribution w/encl: S. Collins, RA M. Dapas, DRA R. Powell, DRP T. Walker, DRP B. Sosa, RI OEDO D. Roberts, NRR R. Ennis, EPU PM, NRR R. Laufer, NRR J. Shea, PM, NRR T. Tate, Backup PM, NRR D. Pelton, DRP, Senior Resident Inspector A. Rancourt, DRP, Resident OA Region I Docket Room (with concurrences)

ROPreports@nrc.gov (All IRs)C:\My Files\Copies\VY IR 2006-03REV1.wpdSUNSI Review Complete: TEW (Reviewer's Initials)After declaring this document "An Official Agency Record" it will be released to the Public.To receive a copy of this document, indicate in the box:

" C" = Copy without attachment/enclosure " E" = Copy withattachment/enclosure " N" = No copyOFFICERI/DRPRI/DRPRI/DRPNAMEDPelton/BES forTWalkerRPowellDATE07/24/0607/24/0607/26/06OFFICIAL RECORD COPY Enclosure iU.S. NUCLEAR REGULATORY COMMISSIONREGION IDocket No.:50-271 Licensee No.:DPR-28 Report No.:05000271/2006003 Licensee:Entergy Nuclear Operations, Inc.

Facility:Vermont Yankee Nuclear Power Station Location:320 Governor Hunt RoadVernon, Vermont 05354-9766Dates:April 1, 2006 through June 30, 2006 Inspectors:David L. Pelton, VY Senior Resident InspectorBeth E. Sienel, VY Resident Inspector Tracy E. Walker, Senior Project Engineer Jennifer A. Bobiak, Reactor Inspector, DRS Patrick W. Finney, Reactor Inspector, DRS James D. Noggle, Senior Health Physicist, DRSApproved by:Raymond J. Powell, ChiefProjects Branch 5 Division of Reactor Projects Enclosure ii

SUMMARY OF FINDINGS

IR 05000271/2006003; 04/01/06 - 06/30/06; Vermont Yankee Nuclear Power Station; RoutineIntegrated Report.This report covered a 13-week period of inspection by resident inspectors and announcedinspections by regional engineering and health physics inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.A.

NRC-Identified and Self-Revealing Findings

No findings of significance were identified.B.Licensee Identified Findings None.

Enclosure

REPORT DETAILS

Summary of Plant StatusVermont Yankee (VY) Nuclear Power Station began the inspection period operating at 87%reactor power. At that time, Entergy personnel were performing power ascension testing activities related to an NRC license amendment authorizing an increase in VY's licensed maximum reactor power level from 1593 megawatts thermal (MWth) to 1912 MWth. On April 1, operators increase power to approximately 91%. Power was again increased to approximately 93% and 96% on April 6 and 22, respectively. On April 28, power was increased to 98%.

On May 5, 2006, operators increased reactor power to the new 100% reactor power limit of 1912 MWth.On May 8, power decreased to approximately 70% during the planned condensate pump triptest performed as part of power ascension testing activities. Following the successful completion of the condensate pump trip test, reactor power was returned to 100% on May 9.

On May 17, operators performed a planned power reduction to approximately 55% to perform individual control rod scram time testing, main steam isolation valve (MSIV) closure testing, turbine valve testing, and rod pattern adjustments. Reactor power was subsequently returned to 100% power on May 21.On May 24, operators reduced reactor power to approximately 58% in response to indicationsof a fire in the east switchgear room and ground faults within the electrical system. This event also resulted in the declaration of an Unusual Event in accordance with Entergy's approved Emergency Plan. (See Section

4OA3 of this report for more details on Entergy's response to

this event.) Following this event, operators maintained reactor power at approximately 80%

pending the completion of necessary repairs to plant equipment. Reactor power was returned to 100% on May 27 where it remained throughout the remainder of the inspection period, with the exception of minor power reductions to support control rod pattern adjustments.1.REACTOR SAFETYCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity1R01Adverse Weather Protection (71111.01).1Readiness for Seasonal Susceptibilities

a. Inspection Scope

(one sample)The inspectors reviewed design features and procedural controls established for theresidual heat removal service water (RHRSW) system to minimize the impact of river silting on the RHRSW system and associated cooling loads (i.e., the residual heatremoval (RHR) system). River silting is a phenomenon typically associated with springtime snow melt and runoff conditions that result in high flow, high silt conditions on the Connecticut River but can also be a concern throughout the year following periods of 2Enclosureheavy rain. The impact of river silt on the RHRSW system is minimized by the siltremoval capability of the service water (SW) system strainers (upstream of the RHRSW system) and by maintaining a minimum flow of water through the RHRSW pump motor cooling lines. The inspectors performed walkdowns of the accessible portions of the RHRSW and SW systems and compared the current system alignments and established RHRSW pump cooling flow to the requirements of Vermont Yankee Operating Procedures (OP) 2124, "Residual Heat Removal System;" OP 2181, "Service Water/Alternate Cooling Operating Procedure;" OP 0150, "Conduct of Operations and Operator Rounds;" Technical Specifications (TS); and the Update Final Safety Analysis Report (UFSAR). The inspectors also reviewed condition reports (CRs) to verify that identified silting and other weather-related issues were entered into the corrective action program and appropriate actions were completed or planned to properly resolve the

issues.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

(71111.04)

a. Inspection Scope

(three samples)The inspectors performed three partial system walkdowns of risk-significant systems toverify system alignment and to identify any discrepancies that could impact system operability. Observed plant conditions were compared to the applicable standby alignment of equipment specified in OP 2124, "Residual Heat Removal System;"

OP 2117, "Standby Gas Treatment;" and OP 2126, "Diesel Generators." The inspectors also observed valve positions, the availability of power supplies, and the general condition of selected components to verify there were no obvious deficiencies.

The inspectors verified the alignment of the following systems:*The "B" train of the RHR system while the "A" train was out of service forplanned maintenance;*The "B" train of the standby gas treatment system while the "A" train was out ofservice for planned maintenance; and*The "B" emergency diesel generator (EDG) while the "A" EDG was out of servicefor planned maintenance.

b. Findings

No findings of significance were identified.

3Enclosure1R05Fire Protection (71111.05Q)

a. Inspection Scope

(nine samples)The inspectors identified fire areas important to plant risk based on a review of Entergy'sVermont Yankee Safe Shutdown Capability Analysis, the Fire Hazards Analysis, and the Individual Plant Examination External Events (IPEEE). The inspectors toured plant areas important to safety in order to verify the suitability of Entergy's control of transient combustibles and ignition sources, and the material condition and operational status of fire protection systems, equipment, and barriers. The following fire areas (FAs) and fire zones (FZs) were inspected.*East Switchgear Room (FA-4);*West Switchgear Room (FA-5);

  • "A" EDG Room (FA-8);
  • "B" EDG Room (FA-9);
  • Cable Vault (FZ-2);
  • Battery Room (FZ-3);
  • Reactor Building, 280 foot elevation, North (FZ RB5);
  • Reactor Building, 280 foot elevation, South (FZ RB6); and
  • Relay House - 345 kilovolt (no fire designation).

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

(71111.06)

a. Inspection Scope

(one sample)The inspectors reviewed Entergy's established flood protection barriers and proceduresfor coping with external flooding events. The inspectors reviewed external flooding information contained in Entergy's IPEEE and compared it to required flooding actions delineated in OP 3127, "Natural Phenomena." The inspectors performed walkdowns of flood-vulnerable areas and ensured equipment needed to mitigate an external flooding event (e.g., sump pumps, floor drain plugs, sand bags, etc.) was available and in working order. The inspectors also reviewed a sample of problems identified in Entergy's corrective action program to verify that Entergy identified and implemented appropriate corrective actions.

b. Findings

No findings of significance were identified.

4Enclosure1R07Heat Sink Performance (71111.07)

a. Inspection Scope

(one sample)The inspectors performed an annual review to verify the readiness of the "A" RHR heatexchanger. The inspectors observed Entergy's execution of biofouling controls for, and inspections of, the "A" RHR heat exchanger including the state of cleanliness of the heat exchanger tubes. Following the completion of these activities, the inspectors performed walkdowns of the "A" RHR heat exchanger to observe inlet and outlet temperatures, primary and secondary side fluid flows, and to look for evidence of leakage.

Observed temperatures and flow rates were compared to expected values contained in OP 2124, "Residual Heat Removal System," the TS, and the UFSAR. The inspectors also reviewed a sample of problems identified in Entergy's corrective action program to verify that Entergy identified and implemented appropriate corrective actions.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

(one sample)The inspectors observed simulator-based licensed operator requalification trainingprovided to operators regarding the expected plant response to a trip of either a feedwater pump or a condensate pump from the new extended power uprate (EPU)100% reactor power level. Training included a discussion of expected plant response(s)and a series of simulator scenarios requiring operators to respond to simulated condensate pump and feedwater pump trips. The inspectors evaluated crew performance in the areas of clarity and formality of communications; ability to take timely actions; prioritization, interpretation, and verification of alarms; procedure use; control board manipulations; oversight and direction from supervisors; and command and control. Crew performance in these areas was compared to Entergy management expectations and guidelines as presented in Vermont Yankee Administrative Procedure (AP) 0151, "Responsibilities and Authorities of Operations Department Personnel;"

AP 0153, "Operations Department Communication and Log Maintenance;" and Vermont Yankee Department Procedure (DP) 0166, "Operations Department Standards."

The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed Entergy evaluators to verify that they also noted the issues to be discussed with the crew.

Additionally, the inspectors observed the fidelity of the plant-specific simulator and compared it to actual plant response(s) and to the requirements of American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.5-1998, "Nuclear Power Plant Simulators for Use in Operator Training and Examination."

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

(71111.12Q)

a. Inspection Scope

(three samples)The inspectors performed three issue/problem-oriented inspections of actions taken byEntergy in response to the inability of operators to fully open "D" SW pump discharge valve SW-2D, the failure of the "A" reactor building-to-torus vacuum breaker to open within in-service testing acceptance criteria during surveillance testing, and the observation of inconsistent closure of an east switchgear room fire damper (FPD-115-12) which is required to close during an actuation of the switchgear room carbon dioxide (CO2) fire suppression system. The inspectors reviewed work practices that may have contributed to degraded system performance, Entergy's ability to identify and address common cause failures, the applicable maintenance rule scoping document for each system, the current classification of these systems in accordance 10 CFR 50.65 (a)(1) or (a)(2), and the appropriateness of the performance criteria and goals established for each system.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment and Emergent Work Evaluation (71111.13)

a. Inspection Scope

(six samples)The inspectors evaluated online risk management for four planned maintenanceactivities and two emergent repair activities. The inspectors reviewed maintenance risk evaluations, work schedules, recent corrective actions, and control room logs to verify that other concurrent or emergent maintenance activities did not significantly increase plant risk. The inspectors compared reviewed items and activities to requirements listed in AP 0125, "Plant Equipment" and AP 0172, "Work Schedule Risk Management -

Online." The inspectors reviewed the following work activities:*Planned maintenance on the "A" train of the RHR system;*Planned maintenance on the "A" EDG;

  • Planned replacement of rod position indicating system (RPIS) power supply,PSX-5;*Planned de-silting of the deep basin which required the safety-related coolingtower cell 2-1 to be taken out of service;*Emergent repair of the "A" reactor building-to-torus vacuum breaker; and

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-Routine Plant Evolutions (71111.14)

a. Inspection Scope

(three samples)The inspectors directly observed and assessed control room operator performanceduring the following non-routine evolutions:*The second of four planned 5% reactor power increases in support of extendedpower uprate on April 1, 2006;*The third of four planned 5% reactor power increases in support of EPU. This 5% increase was broken into two separate 2.5% reactor power increases, performed on April 6 and April 22. The increase was performed in two increments due to a "hold" that had been temporarily placed on EPU testing.

(See Section 4OA5.1 of this report for more detail.); and*The fourth of four planned 5% reactor power increases in support of EPU. This5% increase was also broken into two separate 2.5% reactor power increases, performed on April 28 and May 5. The increase was performed in two increments due to two "holds" that had been placed on EPU testing.

(See Section 4OA5.1 of this report for more detail).The adequacy of personnel performance, procedure compliance, and use of thecorrective action process for all non-routine evolutions were evaluated against the requirements and expectations contained in TS and the following station procedures, as

applicable:*AP 0151, "Responsibilities and Authorities of Operations Department Personnel;"*AP 0153, "Operations Department Communication and Log Maintenance;"

  • DP 0166, "Operations Department Standards;"
  • Engineering Request Special Test Instruction (ERSTI) 04-VY1-1409, "PowerAscension Test Procedure for Extended Power Conditions 1593 to 1912 MWth;"*OP 0105, "Reactor Operations;" and
  • OP 2403, "Control Rod Sequence Exchange with the Reactor Online."

b. Findings

No findings of significance were identified.

7Enclosure1R15Operability Evaluations (71111.15)

a. Inspection Scope

(six samples)The inspectors reviewed six operability determinations prepared by Entergy. The inspectors evaluated the operability determinations against the guidance contained in NRC Inspection Manual, Part 9900, Technical Guidance, "Operability Determinations and Functionality Assessments for Resolution of Degraded or Nonconforming Conditions Adverse to Quality or Safety," as well as Entergy procedure ENN-OP-104, "Operability Determinations." The inspectors verified the adequacy of the following evaluations of degraded or non-conforming conditions:*While testing the mechanical hydraulic pressure control system per ERSTI 04-VY1-1409 at 1832 MWth, a "hold" was placed on testing when Entergy identified steam flow data that exceeded established acceptance criteria;*During the performance of ERSTI 04-VY1-1409, a "hold" was placed on testingwhen operators observed control valve position and steam dome-to-turbine steam chest pressure values that were inconsistent with observed steam flow values;*Inability to fully open "D" SW pump discharge valve SW-2D;

  • RPS/PCIS Agastat relays 5-12C(X) and 5-12D(X) potentially exceeded theirenvironmental qualification lifetime;*Oil leak on the auto transformer (345-to-115 kilovolt transformer that supplies thestartup transformers in the event of a turbine trip); and*"A" EDG jacket water cooling pump leakage.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

(five samples)The inspectors reviewed five post-maintenance testing (PMT) activities on risk-significant systems. The inspectors either directly observed the testing or reviewed completed PMT documentation to verify that the test data met the required acceptance criteria contained in the TS, UFSAR, and inservice testing program. Where testing was directly observed, the inspectors verified that installed test equipment was appropriate and controlled and that the test was performed in accordance with applicable station procedures. The inspectors also verified that the test activities were adequate to ensure system operability and functional capability following maintenance, systems were properly restored following testing, and any discrepancies were appropriately documented in the corrective action program. The inspectors reviewed the following PMT activities:

8Enclosure*Testing in accordance with OP 4124, "Residual Heat Removal and RHR ServiceWater System Surveillance," following planned maintenance on the "A" train of

RHR;*Testing in accordance with work order (WO) 05-2027, following the replacementof RPIS power supply PSX-5;*Testing in accordance with WO 05-5204, following emergent troubleshooting ofthe "A" reactor building-to-torus vacuum breaker;*Testing in accordance with ERT 04-526-03-01, "C51/C52 Breaker and CapacitorBank Functional Test," following the installation of the 115 kilovolt switchyard capacitor banks; and*Testing in accordance with OP 4126, "Diesel Generator Surveillance," followingplanned maintenance on the "A" EDG.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

(71111.22)

a. Inspection Scope

(five samples)The inspectors observed surveillance testing to verify that the test acceptance criteriaspecified for each test was consistent with TS and UFSAR requirements, the test was performed in accordance with the written procedure, the test data was complete and met procedural requirements, and the system was properly returned to service following testing. The inspectors observed selected pre-job briefs for the test activities.

The inspectors also verified that discrepancies were appropriately documented in the corrective action program. The inspectors verified that the following surveillance testing activities met the above requirements:*MSIV quarterly closure testing (in-service test) in accordance with OP 4113,"Main and Auxiliary Steam System Surveillance," Section A; *Core spray pump quarterly operability testing (in-service test) in accordance withOP 4123, "Core Spray System Surveillance," Section C;*SW pump operability and discharge check valve quarterly testing (in-service test)in accordance with OP 4181, "Service Water/Alternate Cooling System Surveillance," Section A;*High pressure coolant injection (HPCI) steam line high flow instrument calibration(routine surveillance) in accordance with OP 4356, "HPCI Steam Line Flow Functional/Calibration," Section B; and*Control rod scram time testing (in-service test) in accordance with OP 4424,"Control Rod Scram Testing and Data Recording," Section B.

b. Findings

No findings of significance were identified.

9Enclosure1R23Temporary Plant Modifications (71111.23)

a. Inspection Scope

(one sample)The inspectors reviewed temporary alteration (TA) 2006-006 made to the circulatingwater system deicing gate to install restraints to hold the gate closed pending installation of a newly designed deicing gate. The deicing gate can be opened during winter conditions to admit a flow of warm, recirculated circulating water from the dischargestructure to the SW intake bay to melt ice buildup.

The original gate guide frame andanchorage had degraded and would no longer support the gate in the closed position. The inspectors compared the information in the TA package to requirements contained in Entergy Nuclear Management Manual Procedure EN-DC-136, "Temporary Alterations." The inspectors observed the installation of the TA and verified that required tags were applied and that the alteration was properly maintained.

b. Findings

No findings of significance were identified.2.RADIATION SAFETYCornerstone: Public Radiation Safety2PS3Radiological Environmental Monitoring Program (REMP) (71122.03)

a. Inspection Scope

(one sample, 02.02.e)During the initial power increase into the EPU range of operation, the inspectorsreviewed the effects on offsite dose with respect to 10 CFR 20.1301(e) and 40 CFR 190 public dose limits. The inspectors witnessed pressurized ion chamber data collection at the highest offsite dose location at the VY fence (location DR-53) on March 5, 2006, during the initial EPU power increase, and again on May 5, 2006 once the 100% EPU power level was reached. Entergy's basis for accurate dose rate measurement and correlations with main steam line radiation monitors were evaluated. This included reviews of applicable procedure and instrument vendor manuals, as well as calibration records for the pressurized ion chamber and main steam line radiation monitor instrumentation. In addition, the licensee's process of data collection, background subtraction, and data reduction was witnessed and reviewed. Inspectors performed an inspection of Entergy's REMP program during the fourth quarter of 2005. During this inspection, unresolved item (URI)05000271/2005005-03, Information Needed to Validate the Direct Dose Calculation Method in Offsite Dose Calculation Manual (ODCM) Section 6.11.1, was opened because additional information was required for the inspectors to determine the adequacy of the direct dose calculation methodology in the ODCM. Since then, an in-office review of the licensee's technical basis for the direct dose calculation methodology contained in Section 6.11.1 of the ODCM was performed with assistance from the NRC's Office of Nuclear Reactor Regulation (NRR).

The 10Enclosurepurpose of the review was to determine whether the calculation was correct andprovided acceptable results to determine dose to the public from VY power operations.

This evaluation was completed on May 16, 2006.

b. Findings

No findings of significance were identified. With the installation of additional turbine shielding on May 17, 2006, the current calculation in Section 6.11.1 of the ODCM is conservative. Entergy plans to conduct another power ascension fence line dose measurement correlation with main steam line radiation monitor measurement at the next outage opportunity and revise Section 6.11.1, accordingly. Inspection and in-office review of this issue has determined that the licensee's offsite dose during EPU operation as determined by the calculation method in the ODCM is adequate and that offsite doses are within the NRC and Environmental Protection Agency (EPA) public dose limits. Based on this inspection and in-office review, Unresolved Item 05000271/2005005-03 is closed.4.OTHER ACTIVITIES4OA1Performance Indicator Verification (71151)

a. Inspection Scope

(two samples)The inspectors sampled Entergy submittals for the two performance indicators (PIs)listed below for the period from April 2004 to March 2006. PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline;"

EN-LI-114, "Performance Indicator Process;" and AP 0094, "NRC Performance Indicator Reporting" were used to verify the basis in reporting for each data element.*Reactor Coolant System Specific Activity; and*Reactor Coolant System Leakage.The inspectors reviewed portions of operator logs and raw PI data developed frommonthly operating reports and discussed the methods for compiling and reporting the PIs with cognizant licensing, operations, and chemistry department personnel.

The inspectors compared graphical representations from the most recent PI report to the raw data to verify that the data was correctly reflected in the report.

b. Findings

No findings of significance were identified.

11Enclosure4OA2Identification and Resolution of Problems (71152).1Review of Items Entered into the Corrective Action Program

a. Inspection Scope

The inspectors routinely reviewed issues during baseline inspection activities and plantstatus reviews to verify they were being entered into Entergy's corrective action program at an appropriate threshold and that adequate attention was being given to timely corrective actions. Additionally, in order to identify repetitive equipment failures and/or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into Entergy's corrective action program. This review was accomplished by reviewing the description of each new CR and/or by attending daily CR screening meetings. A listing of CRs and other documents reviewed is included in the attachment to this report. b.Assessments and ObservationsNo findings of significance were identified.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of Entergy's corrective action program andassociated documents to identify trends that could indicate the existence of a more significant safety issue. The review was focused on human performance-related issues and considered the results of reviews discussed in Section 4OA2.1. The inspectors' review nominally considered the six-month period of January through June 2006. The inspectors compared their results with the results contained in Entergy's quarterly trend report for the first quarter 2006; recently developed "trend" condition reports; Entergy's human performance PI data; and discussions with Operations, Radiation Protection (RP), and Technical Support Department management. The corrective actions assigned to address the individual issues as well as to address human performance trends were reviewed for adequacy. b.Assessment and ObservationsNo findings of significance were identified.

In May 2006, the Operations Manager initiated trending CR 2006-1492 that summarizedtwo recent Operations Department human performance errors. These errors included operator manipulation of an incorrect valve while attempting to remove the "C" condensate demineralizer from service and an operator inadvertently tripping open a breaker associated with the EDGs while hanging a tag on an adjacent breaker. As a result of these errors, the Operations Department Human Performance PI turned Red.

Also in May, the RP manager initiated trending CR 2006-1314 summarizing six recent 12Enclosurehuman performance "precursor" events. For example, an RP technician contaminatedhimself while performing a survey, there were multiple examples of high radiation area entries without a radiological conditions briefing, and a seavan radioactive material container was missing a required lock.Operations Department Management held a "stand down" to brief operating crews onthe individual issues listed in CR 2006-1492 and the apparent trend in human performance errors. Additionally, Operations Department Management plans to develop a human performance improvement plan and to perform focused assessments of human performance-related errors and events. Likewise, RP Department Management held a stand down to brief RP personnel on the individual issues and the trend in human performance error precursors and will continue to maintain a heightened level of awareness to human performance-related issues and events.The inspectors concluded that Operations and RP Department Management madeappropriate use of available tools such as the trending process and the PI process to recognize and take action on low level human performance issues before they became more significant and rose to the level of a finding or violation. However, the inspectors also stressed the need for continued diligence in the area of human performance..3Annual Sample Review - Special Nuclear Material Controls

a. Inspection Scope

(one sample)On April 20, 2004, Entergy determined that two spent fuel rod pieces were not in thestorage location designated in the special nuclear material (SNM) inventory records.

On July 13, 2004, following an investigation, Entergy discovered that the two spent fuel rod pieces were still in the spent fuel pool, but in a different location. In 2004, NRC conducted a special inspection to review Entergy's investigation and conclusions regarding the search for the two spent fuel rod pieces (Inspection Report 05000271/2004007, dated December 2, 2004). On June 22, 2005, NRC issued a Severity Level III Notice of Violation with no civil penalty to Entergy for failure to keep adequate records of the SNM in its possession and failure to conduct adequate physical inventories (EA 04-0174). The purpose of this inspection was to review the corrective actions taken by Entergy toaddress the identified root causes of the failure to account for the spent fuel rod pieces.

The inspectors reviewed the corrective actions completed since September 2004, and assessed the effectiveness of the corrective actions in addressing the identified causes of the event. Specifically, the inspectors reviewed CRs associated with the misplaced spent fuel rod pieces, and other CRs associated with SNM controls initiated since September 2004. The inspectors also reviewed assessments of SNM controls performed by Entergy. The inspector reviewed procedures for control of SNM that had been revised to address the causes of the event, and reviewed records of SNM inventories completed since September 2004. The inspector also toured the refuel floor and held discussions with reactor engineering personnel.

b. Findings and Observations

No findings of significance were identified. The inspectors found that Entergy had taken significant actions to improve SNM controlssince the event in 2004. Procedures were revised and processes were changed to establish detailed controls for transfer and tracking of SNM with an appropriate level of management oversight. There were two instances in which tamper seals for SNM containers were found broken (no material was misplaced) in 2004 and 2005. In both cases, Entergy appropriately considered the effectiveness of previous corrective actions and took further actions to prevent recurrence. Entergy had performed several assessments of SNM controls since the loss ofaccountability of the fuel rod pieces in 2004. The inspectors questioned the timing of the licensee's effectiveness review of the corrective actions for the event because, at the time it was performed in June 2005, no fuel transfers had been performed and the 2005 annual inventory had not yet been conducted. Although the effectiveness review was not performance based, a Quality Assurance (QA) surveillance was subsequently performed which included observations of SNM transfers during refueling outage (RFO)25 and conduct of the 2005 annual inventory. Entergy also conducted a self-assessment of SNM controls during RFO 25 and the 2005 annual inventory, and a corporate assessment of SNM controls at Vermont Yankee was completed in early

2006.Based on the results of this inspection, VIO 05000271/2004007-01, "Did Not KeepAdequate Records, Follow Procedures, and Perform Physical Inventory of Special Nuclear Material," (EA 04-0174) is closed..4Annual Sample: Failure of Emergency Diesel Generator Loss of Field Relays

a. Inspection Scope

(one sample)The inspectors reviewed Entergy's corrective actions in response to CR 2005-3854,"DG-1-1A and DG-1-1B loss of field relays may not adequately protect the EDGs during a loss of field event when operating in parallel with the grid." The inspectors reviewed CRs, night orders, work orders, plant drawings and engineering documentation as listed in the attachment to this report. The inspectors also performed walkdowns of the EDGs and interviewed operations and engineering department personnel to determine if Entergy had adequately resolved the issues.

b. Findings and Observations

No findings of significance were identified.

Entergy's identification of the cause of the "B" emergency diesel generator failure andthe associated corrective actions were appropriate. However, the inspectors identified that an interim administrative control measure was not maintained to ensure that the 14EnclosureEDGs were appropriately secured during a loss of field event while paralleled with offsitepower or the main generator. An entry was originally made in the Operations Night Orders shortly after identification of the issue (November 2005) that alerted operators to the lack of field-loss protection. This entry reminded operators to monitor field volts and output voltage during surveillance testing, to trip the EDG immediately upon indication of an EDG loss of field, and that the preferred method for tripping the EDG was by using the Test switch in the main control room. The inspectors identified that the entry was removed from the Night Orders on approximately February 16, 2006, without transferal to another administrative process despite the continuing lack of protection.

Modifications to the EDG loss of field relays are scheduled to occur later in 2006.

Entergy entered this issue into their corrective action program (CR 2006-1438) and incorporated the information into the pre-job briefing form used during monthly EDG surveillances. This finding was minor because operators had received licensed operator requalification training on the November 2005 EDG event, which included the associated operator responses, and operating procedures were in place to take appropriate emergency actions in the case of abnormal EDG performance.4OA3Event Followup (71153).1Indications of a Fire in the East Switchgear Room and the Declaration of an UnusualEvent

a. Inspection Scope

(one sample)The inspectors responded to the site following the declaration of an Unusual Event (UE)on May 24. The UE was declared on the basis of indications of an in-plant fire that was not extinguished within 10 minutes. The inspectors observed reactor plant parameters in the control room and evaluated safety system response to the event. The inspectors also assessed the response of the licensed operators against applicable operating procedures, abnormal operating procedures, and emergency operating procedures.

The inspectors evaluated Entergy's classification of the event as a UE against the Emergency Plan Emergency Action Level (EAL) procedures and the ability of emergency response staff to notify NRC and State/Local Governments as required.

The inspectors also evaluated the response of Entergy's fire brigade and the east switchgear room automatic fire protection systems.

b. Findings

The event appears to have been initiated by a ground fault that developed in thewindings of the "C" condensate pump motor. The resultant fault current was transferred, by design, to a resistor bank located in the east switchgear room on bus 2.

This resistor bank is designed to dissipate the current generated during a ground fault in the form of heat. Initial fire brigade reports from the east switchgear room indicated that there were no signs of flames or smoke in the vicinity of the "C" condensate pump breaker. However, the heat generated by the resistor bank appears to have been sufficient to have ionized dust that had accumulated on and around the resistor bank.

15EnclosureIt is believed that the ionized dust caused adjacent fire detectors to alarm and actuatethe automatic CO2 fire suppression system. Similar switchgear room CO2 discharge events occurred at VY during motor ground faults in 1983 and 1989. As of the conclusion of this inspection, Entergy had not completed their root cause analysis of this event. Additionally, the inspectors continue to review internal and external operating experience (OE) related to pump motor ground faults, large motor preventive maintenance, and adverse effects of dust accumulation on electrical equipment.

Pending the completion of the inspectors review of Entergy's root cause analysis and applicable OE, these issues are considered to be an unresolved item (URI):

URI 0500271/2006003-01, Condensate Pump Motor Fault and Switchgear Room CO2 Initiation Result in the Declaration of an Unusual Event.4OA5Other.1Power Uprate: Power Ascension Testing (71004)

a. Inspection Scope

(four samples)The inspectors observed power ascension testing performed in accordance withattachments to test procedure ERSTI-04-VY1-1409. The four inspection samples comprised level and pressure testing at 1752, 1832, and 1912 MWth as well as a condensate pump trip test conducted within 7 days of reaching 1912 MWth. The inspectors observed testing to verify that the test acceptance criteria specified was consistent with TS and UFSAR requirements, the test was performed in accordance with the written procedure, test data was complete and met procedural requirements, and affected systems were properly returned to service following testing.

The inspectors also observed selected testing pre-job briefs. The inspectors verified that discrepancies identified during testing were appropriately documented in the corrective action program. The inspectors verified that the following testing activities met the above requirements:*Testing at 1752 MWth Attachment 7B, "Feedwater Level Changes 1752 MWth" 8B, "MHC [mechanical hydraulic control] Pressure Change Demonstration 1752 MWth"*Testing at 1832 MWthAttachment 7C, "Feedwater Level Changes 1832 MWth" 8C, "MHC Pressure Change Demonstration 1832 MWth"*Testing at 1912 MWthAttachment 7D, "Feedwater Level Changes 1912 MWth" 8D, "MHC Pressure Change Demonstration 1912 MWth"*Condensate Pump Trip TestingAttachment 18, "Condensate Pump Trip Test at Full EPU Power"At 1793 MWth, 1832 MWth, and 1872 MWth, the licensee identified conditions that metLevel 2 acceptance criteria established in ERSTI-04-VY1-1409 and required a "hold" be placed on further testing pending review of the data by Engineering Department 16Enclosurepersonnel and NRC staff, as appropriate. The conditions identified included "A" mainsteam line strain gage data that exceeded acceptance criteria at 1793 MWth; steam flow indication variability that exceeded acceptance criteria and operator-observed inconsistencies between indicated steam flow, control valve position, and steam system differential pressure at 1832 MWth; and moisture carryover acceptance criteria was exceeded at 1872 MWth. For each of the "holds" placed on testing, the inspectors ensured Entergy had entered the issues into their corrective action program and had appropriately evaluated the condition(s) prior to continuing with testing. NRC headquarters staff also reviewed selected issues prior to continuing with testing.

Section 1R15 of this report discusses inspections of the steam flow indication variability and observed inconsistencies between indicated steam flow, control valve position, and steam system differential pressure since these conditions did not specifically require NRC headquarters staff review prior to continuing with testing.At 1752 MWth and 1912 MWth, the inspectors performed walkdowns of the feedwaterheaters, the main condenser and moisture separators, and main steam system piping and valves. The inspectors looked for visual evidence of water and steam leaks and equipment vibration.

b. Findings

No findings of significance were identified..2(Closed) URI 05000271/2006002-01: Training Provided to Licensed OperatorsRegarding Plant Response to a Condensate Pump TripDuring the observation of training initially provided to licensed operators on the expectedplant response to a trip of a condensate pump from 100% reactor power, the inspectors noted that the simulated plant response differed from the predicted plant response indicated in Reactor Engineering's analysis for this event. The difference was in the final values of core thermal power and core flow immediately following the pump trip.

At that time, the inspectors were concerned that the condensate pump trip training initially provided to licensed operators did not meet the met the guidance outlined in American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.5-1998, "Nuclear Power Plant Simulators for Use in Operator Training and Examination." Based on the results of the inspections of licensed operator training discussed in Section 1R11 and on the results of the inspections of the condensate pump trip test discussed in Section 4OA5.1, the inspectors concluded that the condensate pump trip training provided to licensed operators met the guidance outlined in ANSI/ANS-3.5-1998.

This URI is closed.

17Enclosure

.3 (Closed) NRC Temporary Instruction (TI) 2515/165, "Operational Readiness of OffsitePower and Impact on Plant Risk

"

a. Inspection Scope

The objective of TI 2515/165, "Operational Readiness of Offsite Power and Impact onPlant Risk," was to gather information to support the assessment of nuclear power plant operational readiness of offsite power systems and impact on plant risk. The inspectors evaluated licensee procedures against the specific offsite power, risk assessment and system grid reliability requirements of TI 2515/165. They also discussed the attributes with licensee personnel. The information gathered while completing this TI was forwarded to the Office ofNuclear Reactor Regulation for further review and evaluation on April 3, 2006.

b. Findings

No findings of significance were identified..4Institute of Nuclear Power Operations (INPO)/World Association of Nuclear Operators(WANO) Plant Assessment Report ReviewThe inspectors reviewed the final report for the INPO/WANO plant assessment of theVermont Yankee Power Station conducted in April 2005. The inspectors reviewed the report to ensure that issues identified were consistent with the NRC perspectives of Entergy's performance and to verify if any significant safety issues were identified that required further NRC follow-up.4OA6Meetings, Including ExitExit Meeting Summary On July 12, the resident inspectors presented the inspection results to Messrs. BillMaguire and John Dreyfuss and members of the VY staff. The inspectors askedwhether any materials examined during the inspection should be considered proprietary.

No proprietary information was identified.ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Entergy Personnel

J. Devincentis, Licensing Manager
J. Dreyfuss, Director of Engineering
M. Hamer, Licensing
W. Maguire, General Manager of Plant Operations
K. Pushee, Radiation Protection Manager
N. Rademacher, Director of Nuclear Safety
J. Thayer, Site Vice President (former)
T. Sullivan, Site Vice President (current)

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened05000271/2006003-01URICondensate Pump Motor Fault and Switchgear Room CO2Initiation Result in the Declaration of an Unusual Event

(Section 4OA3.1)

Closed

05000271/2004007-01VIODid Not Keep Adequate Records, Follow Procedures, andPerform Physical Inventory of Special Nuclear Material

(Section 4OA2.3)05000271/2005005-03URIInformation Needed to Validate the Direct DoseCalculation Method in ODCM Section 6.11.1

(Section 2PS3)05000271/2006002-01URITraining Provided to Licensed Operators Regarding PlantResponse to a Condensate Pump Trip (Section 4OA5.2)

LIST OF DOCUMENTS REVIEWED

Section 2PS3:

Radiological Environmental Monitoring Program ProceduresOP 4505Source Calibration of Main Steam Line Radiation MonitorsOP 4658Periodic Evaluation of Direct Dose From Plant Operation