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=Text=
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{{#Wiki_filter:__ _.           .     . .       . _.. _.             .                       ..       - ..
{{#Wiki_filter:__ _.
      . ."                                                                           y dhu)
.
'
. .
                                                    FE8 051987
. _..
            Docket Nos. 50-269, 50-270, 50-287                                                                   !
_.
j           License Nos. DPR-38, DPR-47, DPR-55                                         .
.
            Duke Power Company
..
          96TN: Mr. H. B. Tucker, Vice President
- ..
                    Nuclear Production Department
. ."
j           422 South Church Street                                                                               '
y dhu)
            Charlotte, NC 28242
'
            Gentlemen:
FE8 051987
                                                                                                                  ;
Docket Nos. 50-269, 50-270, 50-287
  '
!
            SUBJECT: NOTICE OF VIOLATION
j
]                       (INSPECTION REPORT NOS. 50-269/86-33, 50-270/86-33 AND 50-287/86-33)
License Nos. DPR-38, DPR-47, DPR-55
                                                                                                                  ,
.
!         This refers to the Nuclear Regulatory Commission (NRC) inspection conducted on.                       L
Duke Power Company
!         October 15 - November 10, 1986. The inspection included a review of activities-                       '
96TN: Mr. H. B. Tucker, Vice President
(         authorized for your Oconee facility. At the conclusion of the inspection, the
Nuclear Production Department
j
422 South Church Street
'
Charlotte, NC 28242
Gentlemen:
;
'
SUBJECT: NOTICE OF VIOLATION
]
(INSPECTION REPORT NOS. 50-269/86-33, 50-270/86-33 AND 50-287/86-33)
,
!
This refers to the Nuclear Regulatory Commission (NRC) inspection conducted on.
L
!
October 15 - November 10, 1986. The inspection included a review of activities-
'
(
authorized for your Oconee facility. At the conclusion of the inspection, the
findings were discussed with those members of your staff identified in'the.
-
-
            findings were discussed with those members of your staff identified in'the.
previously forwarded inspection report. The report documenting-this inspection
            previously forwarded inspection report. The report documenting-this inspection                       '
;
;           was sent to you with a letter dated December 1, 1986. NRC concerns relative to
was sent to you with a letter dated December 1, 1986. NRC concerns relative to
i           the inspection findings were discussed by Dr. J. N. Grace Regional Administrator,
'
i           NRC, Region II, with you and members of your staff in an Enforcement Conference                       '
i
;           held on December 22, 1986.                                                                           -
the inspection findings were discussed by Dr. J. N. Grace Regional Administrator,
!           The inspection findings indicate that certain. activities appeared to violate NRC
i
1           requirements. The violation, references to pertinent requirements, and elements
NRC, Region II, with you and members of your staff in an Enforcement Conference
;           to be included in your response are described in the enclosed Notice of Violation.
'
            The violation described in the enclosed Notice of Violation involved a failure
;
            to satisfy a Technical Specification Limiting Condition for_0peration which .
held on December 22, 1986.
-
!
The inspection findings indicate that certain. activities appeared to violate NRC
1
requirements. The violation, references to pertinent requirements, and elements
;
to be included in your response are described in the enclosed Notice of Violation.
The violation described in the enclosed Notice of Violation involved a failure
'
to satisfy a Technical Specification Limiting Condition for_0peration which .
-;
l
required the Emergency Condenser Cooling Water _(ECCW) system to be maintained in
,
;
an operable condition. The violation resulted from inadequate . surveillance .
j
testing to detect degradation of the ECCW system. As discovered during a test
1
i
conducted on October 1,1986, because of air inleakage, the ECCW system was not .
j
able to perform its required function of providing sustained siphon flow through
the main condenser during a station blackout with the level of Lake Keowee nine
'i
feet below full pond. Although the system had been tested _according to the
procedure and at the required frequency, the test procedure:was inadequate to
reveal the system deficiencies.
:
.The ECCW system would be inoperable under the' conditions of the loss of all
~
off-site and on-site power (station blackout) coincident with a low level in
'
'
                                                                                                                -;
l          required the Emergency Condenser Cooling Water _(ECCW) system to be maintained in                    ,
;          an operable condition. The violation resulted from inadequate . surveillance .
j          testing to detect degradation of the ECCW system. As discovered during a test                        1
i          conducted on October 1,1986, because of air inleakage, the ECCW system was not .
j          able to perform its required function of providing sustained siphon flow through
            the main condenser during a station blackout with the level of Lake Keowee nine                    'i
            feet below full pond. Although the system had been tested _according to the
            procedure and at the required frequency, the test procedure:was inadequate to
            reveal the system deficiencies.
:          .The ECCW system would be inoperable under the' conditions of the loss of all                        ~
            off-site and on-site power (station blackout) coincident with a low level in                          '
1
1
Lake Keowee. Because under other conditions, suchlas a loss of just off-site
~
~
            Lake Keowee. Because under other conditions, suchlas a loss of just off-site
power, the ECCW system remains operable, and the fact that sufficient water
            power, the ECCW system remains operable, and the fact that sufficient water                           i
i
            supplies exist to provide decay heat removal even without the operation of the                         '
'
j           ECCW system, this violation is considered to be of low safety significance.
supplies exist to provide decay heat removal even without the operation of the
j
ECCW system, this violation is considered to be of low safety significance.
In accordance with the " General Statement of. Policy and Procedure for NRC
"
"
            In accordance with the " General Statement of. Policy and Procedure for NRC
Enforcement Action," 10 CFR- Part 2 Appendix C (1986),' the violation described
            Enforcement Action," 10 CFR- Part 2 Appendix C (1986),' the violation described
[
[           in the enclosed Notice has been categorized as a Severity Level IV violation.~.
in the enclosed Notice has been categorized as a Severity Level IV violation.~.
I
I
;-           8702180438 870205
;-
              PDR     ADOCK 05000269
8702180438 870205
              G                   PDR
PDR
JH,                                                                                        l   I y T61-
ADOCK 05000269
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    .
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.-
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        Duke Power Company                       2
FE8 05 387
                                                                          FE8 05 387
Duke Power Company
        Although the violation was identified by the licensee with the resident
2
        inspectors present, the discovery of the degradation of.the ECCW system was   ;
Although the violation was identified by the licensee with the resident
        considered not to have been a part of the test as originally planned and       1
inspectors present, the discovery of the degradation of.the ECCW system was
        previously performed and was discovered fortuitously because the test being
;
        conducted lasted longer than anticipated. Previous testing had not identified
considered not to have been a part of the test as originally planned and
        the ECCW system degradation. Therefore, this violation is being cited.
1
        In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2
previously performed and was discovered fortuitously because the test being
        Title 10, Code of Federal Regulations, a copy of this letter and its enclosure
conducted lasted longer than anticipated. Previous testing had not identified
        will be placed in the NRC Public Document Room.
the ECCW system degradation. Therefore, this violation is being cited.
        The responses directed by this letter and its enclosure are not subject to the
In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2
        clearance procedures of the Office of Management and Budget as required by the
Title 10, Code of Federal Regulations, a copy of this letter and its enclosure
        Paperwork Reduction Act of 1980 PL 96-511.
will be placed in the NRC Public Document Room.
        Should you have any questions concerning this letter, please' contact us.
The responses directed by this letter and its enclosure are not subject to the
                                                  Sincerely,
clearance procedures of the Office of Management and Budget as required by the
                                                    Original signed by
Paperwork Reduction Act of 1980 PL 96-511.
                                                      J. P. Stohr/for -
Should you have any questions concerning this letter, please' contact us.
                                                  J. Nelson Grace
Sincerely,
                                                  Regional Administrator
Original signed by
        Enclosure:
J. P. Stohr/for -
        Notice of Violation                                                       '
J. Nelson Grace
        cc w/ encl:
Regional Administrator
  @.S.Tuckman,StationManager
Enclosure:
        bec w/ encl:
Notice of Violation
      LNRC Resident Inspector
'
    p.Nicolaras,NRR
cc w/ encl:
  t,df. Beach, ES:HQ
@.S.Tuckman,StationManager
        G. Jenkins, EICS
bec w/ encl:
        L. Reyes, DRP
LNRC Resident Inspector
        A. Gibson DRS
p.Nicolaras,NRR
        DocumentdontrolDesk
t,df. Beach, ES:HQ
        State of North Carolina
G. Jenkins, EICS
        IE: S                   DRS   I
L. Reyes, DRP
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A. Gibson DRS
        Beach                   Reyes           GR enk s             MWr
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State of North Carolina
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Latest revision as of 13:59, 23 May 2025

Discusses Insp Repts 50-269/86-33,50-270/86-33 & 50-287/86-33 on 861015-1110 & Forwards Notice of Violation. Test Procedure for Emergency Condenser Cooling Water Sys Inadequate to Reveal Sys Deficiencies
ML20210U294
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 02/05/1987
From: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Tucker H
DUKE POWER CO.
Shared Package
ML20210U296 List:
References
NUDOCS 8702180438
Download: ML20210U294 (2)


See also: IR 05000269/1986033

Text

__ _.

.

. .

. _..

_.

.

..

- ..

. ."

y dhu)

'

FE8 051987

Docket Nos. 50-269, 50-270, 50-287

!

j

License Nos. DPR-38, DPR-47, DPR-55

.

Duke Power Company

96TN: Mr. H. B. Tucker, Vice President

Nuclear Production Department

j

422 South Church Street

'

Charlotte, NC 28242

Gentlemen:

'

SUBJECT: NOTICE OF VIOLATION

]

(INSPECTION REPORT NOS. 50-269/86-33, 50-270/86-33 AND 50-287/86-33)

,

!

This refers to the Nuclear Regulatory Commission (NRC) inspection conducted on.

L

!

October 15 - November 10, 1986. The inspection included a review of activities-

'

(

authorized for your Oconee facility. At the conclusion of the inspection, the

findings were discussed with those members of your staff identified in'the.

-

previously forwarded inspection report. The report documenting-this inspection

was sent to you with a letter dated December 1, 1986. NRC concerns relative to

'

i

the inspection findings were discussed by Dr. J. N. Grace Regional Administrator,

i

NRC, Region II, with you and members of your staff in an Enforcement Conference

'

held on December 22, 1986.

-

!

The inspection findings indicate that certain. activities appeared to violate NRC

1

requirements. The violation, references to pertinent requirements, and elements

to be included in your response are described in the enclosed Notice of Violation.

The violation described in the enclosed Notice of Violation involved a failure

'

to satisfy a Technical Specification Limiting Condition for_0peration which .

-;

l

required the Emergency Condenser Cooling Water _(ECCW) system to be maintained in

,

an operable condition. The violation resulted from inadequate . surveillance .

j

testing to detect degradation of the ECCW system. As discovered during a test

1

i

conducted on October 1,1986, because of air inleakage, the ECCW system was not .

j

able to perform its required function of providing sustained siphon flow through

the main condenser during a station blackout with the level of Lake Keowee nine

'i

feet below full pond. Although the system had been tested _according to the

procedure and at the required frequency, the test procedure:was inadequate to

reveal the system deficiencies.

.The ECCW system would be inoperable under the' conditions of the loss of all

~

off-site and on-site power (station blackout) coincident with a low level in

'

1

Lake Keowee. Because under other conditions, suchlas a loss of just off-site

~

power, the ECCW system remains operable, and the fact that sufficient water

i

'

supplies exist to provide decay heat removal even without the operation of the

j

ECCW system, this violation is considered to be of low safety significance.

In accordance with the " General Statement of. Policy and Procedure for NRC

"

Enforcement Action," 10 CFR- Part 2 Appendix C (1986),' the violation described

[

in the enclosed Notice has been categorized as a Severity Level IV violation.~.

I

-

8702180438 870205

PDR

ADOCK 05000269

G

PDR

l I y T61-

JH,

_

.

1

.

.

c

. .

.

. -

...

_-

-

m..,

. .a

'

.

.-

FE8 05 387

Duke Power Company

2

Although the violation was identified by the licensee with the resident

inspectors present, the discovery of the degradation of.the ECCW system was

considered not to have been a part of the test as originally planned and

1

previously performed and was discovered fortuitously because the test being

conducted lasted longer than anticipated. Previous testing had not identified

the ECCW system degradation. Therefore, this violation is being cited.

In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2

Title 10, Code of Federal Regulations, a copy of this letter and its enclosure

will be placed in the NRC Public Document Room.

The responses directed by this letter and its enclosure are not subject to the

clearance procedures of the Office of Management and Budget as required by the

Paperwork Reduction Act of 1980 PL 96-511.

Should you have any questions concerning this letter, please' contact us.

Sincerely,

Original signed by

J. P. Stohr/for -

J. Nelson Grace

Regional Administrator

Enclosure:

Notice of Violation

'

cc w/ encl:

@.S.Tuckman,StationManager

bec w/ encl:

LNRC Resident Inspector

p.Nicolaras,NRR

t,df. Beach, ES:HQ

G. Jenkins, EICS

L. Reyes, DRP

A. Gibson DRS

DocumentdontrolDesk

State of North Carolina

If

IE: S

DRS

I

EI(S

OR

Beach

Reyes

GR enk s

MWr st

J

,

2/3 /87

2/.f /87

2/,f/7

2/ 5 /87

6 20

.