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If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding. | If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding. | ||
Sincerely, | Sincerely, Neil F. O'Keefe, Chief Reactor Projects Branch B Division of Reactor Projects | ||
Neil F. O'Keefe, Chief Reactor Projects Branch B Division of Reactor Projects Docket Nos. 05000445 and 05000446 License Nos. NPF-87 and NPF-89 | |||
Docket Nos. 05000445 and 05000446 License Nos. NPF-87 and NPF-89 | |||
===Enclosure:=== | ===Enclosure:=== | ||
As stated | As stated | ||
==Inspection Report== | ==Inspection Report== | ||
Docket Numbers: 05000445 and 05000446 License Numbers: NPF-87 and NPF-89 Report Numbers: 05000445/2020001 and 05000446/2020001 Enterprise Identifier: I-2020-001-0010 Licensee: VISTRA Operations Company, LLC Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2 Location: Glen Rose, TX 76043 Inspection Dates: January 1 to March 31, 2020 Inspectors: J. Ellegood, Senior Resident Inspector D. Antonangeli, Health Physicist B. Baca, Health Physicist N. Day, Resident Inspector N. Greene, Senior Health Physicist J. Melfi, Project Engineer J. O'Donnell, Senior Health Physicist Approved By: Neil F. O'Keefe, Chief Reactor Projects Branch B Division of Reactor Projects | Docket Numbers: | ||
05000445 and 05000446 | |||
License Numbers: | |||
NPF-87 and NPF-89 | |||
Report Numbers: | |||
05000445/2020001 and 05000446/2020001 | |||
Enterprise Identifier: I-2020-001-0010 | |||
Licensee: | |||
VISTRA Operations Company, LLC | |||
Facility: | |||
Comanche Peak Nuclear Power Plant, Units 1 and 2 | |||
Location: | |||
Glen Rose, TX 76043 | |||
Inspection Dates: | |||
January 1 to March 31, 2020 | |||
Inspectors: | |||
J. Ellegood, Senior Resident Inspector | |||
D. Antonangeli, Health Physicist | |||
B. Baca, Health Physicist | |||
N. Day, Resident Inspector | |||
N. Greene, Senior Health Physicist | |||
J. Melfi, Project Engineer | |||
J. O'Donnell, Senior Health Physicist | |||
Approved By: | |||
Neil F. O'Keefe, Chief | |||
Reactor Projects Branch B | |||
Division of Reactor Projects | |||
=SUMMARY= | =SUMMARY= | ||
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===List of Findings and Violations=== | ===List of Findings and Violations=== | ||
Manual Reactor Trip Due to Loss of both Main Feed Pumps Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000446/2020001-01 Open/Closed | |||
Manual Reactor Trip Due to Loss of both Main Feed Pumps Cornerstone | [H.12] - Avoid Complacency 71153 A self-revealed finding and associated non-cited violation (NCV) of very low safety significance occurred when the licensee failed to implement procedures for operation of the feed and condensate system as required by Technical Specification 5.4.1.a. Specifically, while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the operators isolated circulating water flow to the condensers, causing a loss of both Unit 2 main feedwater pumps. Control room operators manually insert a plant trip in response to the loss of feedwater. | ||
===Additional Tracking Items=== | ===Additional Tracking Items=== | ||
Type | Type Issue Number Title Report Section Status LER 05000446/2018-002-01 LER 2018-002-01 for Comanche Peak, Unit 2, | ||
Automatic Actuation of Auxiliary Feedwater System. | Automatic Actuation of Auxiliary Feedwater System. | ||
LER | 71153 Closed LER 05000446/2019-002-00 LER 2019-002-00 for Comanche Peak Nuclear Power Plant, Unit 2, | ||
Automatic Actuation of Auxiliary Feedwater System. | Automatic Actuation of Auxiliary Feedwater System. | ||
71153 Closed | |||
=PLANT STATUS= | =PLANT STATUS= | ||
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==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
==71111.01 - Adverse Weather Protection== | |||
==71111.01 - Adverse Weather Protection Impending Severe Weather Sample (IP Section 03.02) == | ===Impending Severe Weather Sample (IP Section 03.02) (1 Sample)=== | ||
: (1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from forecasted thunderstorms on January 10, 2020 | : (1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from forecasted thunderstorms on January 10, 2020 | ||
==71111.04 - Equipment Alignment Partial Walkdown Sample (IP Section 03.01) == | ==71111.04 - Equipment Alignment== | ||
===Partial Walkdown Sample (IP Section 03.01) (1 Sample)=== | |||
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains: | The inspectors evaluated system configurations during partial walkdowns of the following systems/trains: | ||
: (1) Unit 2, chemical and volume control system on February 6, 2020 | : (1) Unit 2, chemical and volume control system on February 6, 2020 | ||
==71111.05 - Fire Protection Fire Area Walkdown and Inspection Sample (IP Section 03.01) == | ==71111.05 - Fire Protection== | ||
===Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)=== | |||
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas: | The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas: | ||
: (1) Unit 1, turbine building basement on January 17, 2020 | : (1) Unit 1, turbine building basement on January 17, 2020 | ||
: (2) Unit 2, turbine building basement on January 17, 2020 | : (2) Unit 2, turbine building basement on January 17, 2020 | ||
: (3) Unit 2, emergency diesel generator A room on January 23, 2020 | : (3) Unit 2, emergency diesel generator A room on January 23, 2020 | ||
: (4) Service water intake structure building on March 26, 2020 | : (4) Service water intake structure building on March 26, 2020 | ||
===Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)=== | ===Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)=== | ||
: (1) The inspectors evaluated the onsite fire brigade training and performance during an | : (1) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill on March 3, 2020 | ||
==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance== | ==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance== | ||
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample) | Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample) | ||
: (1) The inspectors observed and evaluated licensed operator performance in the control room during turbine start and synchronization to the grid on January 3, 2020 | : (1) The inspectors observed and evaluated licensed operator performance in the control room during turbine start and synchronization to the grid on January 3, 2020 | ||
===Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)=== | ===Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)=== | ||
: (1) The inspectors observed and evaluated licensed operators for just in time training for | : (1) The inspectors observed and evaluated licensed operators for just in time training for a reactor startup on January 2, 2020 | ||
==71111.12 - Maintenance Effectiveness== | |||
===Maintenance Effectiveness (IP Section 03.01) (1 Sample)=== | |||
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function: | The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function: | ||
: (1) Unit 2, auxiliary feedwater system on February 25, 2020 | : (1) Unit 2, auxiliary feedwater system on February 25, 2020 | ||
==71111.13 - Maintenance Risk Assessments and Emergent Work Control== | ==71111.13 - Maintenance Risk Assessments and Emergent Work Control== | ||
===Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)=== | ===Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)=== | ||
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed; | The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed; | ||
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==71111.15 - Operability Determinations and Functionality Assessments== | ==71111.15 - Operability Determinations and Functionality Assessments== | ||
===Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)=== | ===Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)=== | ||
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments: | The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments: | ||
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: (4) Unit 2, control rods from potential thermal sleeve cracking as described in Part 21 report LTR-NRC-19-79, and corrective action document TR 2020-1247 | : (4) Unit 2, control rods from potential thermal sleeve cracking as described in Part 21 report LTR-NRC-19-79, and corrective action document TR 2020-1247 | ||
==71111.19 - Post-Maintenance Testing Post-Maintenance Test Sample (IP Section 03.01) == | ==71111.19 - Post-Maintenance Testing== | ||
===Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)=== | |||
The inspectors evaluated the following post maintenance test activities to verify system operability and functionality: | The inspectors evaluated the following post maintenance test activities to verify system operability and functionality: | ||
: (1) Repair of disconnected wires and replacement of components in the Unit 2 safeguard sequencer system per Work Order 5840776 on February 20, 2020 | : (1) Repair of disconnected wires and replacement of components in the Unit 2 safeguard sequencer system per Work Order 5840776 on February 20, 2020 | ||
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: (4) As found testing, calibration, and installation of Unit 2 safeguard sequencer B undervoltage relays per Work Order 5666818 on March 4, 2020. | : (4) As found testing, calibration, and installation of Unit 2 safeguard sequencer B undervoltage relays per Work Order 5666818 on March 4, 2020. | ||
==71111.20 - Refueling and Other Outage Activities Refueling/Other Outage Sample (IP Section 03.01) == | ==71111.20 - Refueling and Other Outage Activities== | ||
===Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)=== | |||
: (1) The inspectors evaluated licensee activities during a Unit 2 unplanned outage from January 1-3, 2020. | : (1) The inspectors evaluated licensee activities during a Unit 2 unplanned outage from January 1-3, 2020. | ||
==71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests: | ==71111.22 - Surveillance Testing== | ||
The inspectors evaluated the following surveillance tests: | |||
===Surveillance Tests (other) (IP Section 03.01) | ===Surveillance Tests (other) (IP Section 03.01)=== | ||
{{IP sample|IP=IP 71111.22|count=4}} | |||
: (1) Unit 2, emergency diesel generator monthly load test per Procedure OPT 214B, Diesel Generator Operability Test, Revision 16, on January 22, 2020 | : (1) Unit 2, emergency diesel generator monthly load test per Procedure OPT 214B, Diesel Generator Operability Test, Revision 16, on January 22, 2020 | ||
: (2) Unit 2, at power end of core life reactivity test per Work Order 5659452 on February 10, 2020 | : (2) Unit 2, at power end of core life reactivity test per Work Order 5659452 on February 10, 2020 | ||
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==71114.06 - Drill Evaluation== | ==71114.06 - Drill Evaluation== | ||
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample) | |||
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) | |||
(1 Sample) | |||
: (1) The blue team emergency preparedness drill on February 19, | : (1) The blue team emergency preparedness drill on February 19, | ||
==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
==71124.05 - Radiation Monitoring Instrumentation== | |||
==71124.05 - Radiation Monitoring Instrumentation Walk Downs and Observations (IP Section 02.01) == | ===Walk Downs and Observations (IP Section 02.01) (1 Sample)=== | ||
The inspectors evaluated the following radiation detection instrumentation during plant walkdowns: | The inspectors evaluated the following radiation detection instrumentation during plant walkdowns: | ||
: (1) Portable Survey Instruments | : (1) Portable Survey Instruments | ||
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* RM-177, HP-1026 | * RM-177, HP-1026 | ||
* AMS-4, HP-2166 | * AMS-4, HP-2166 | ||
* 3030E, HP-3270 Source Check Demonstration | * 3030E, HP-3270 | ||
Source Check Demonstration | |||
* Rad Eye G, HP-3112 | * Rad Eye G, HP-3112 | ||
* Telepole, HP-1906 | * Telepole, HP-1906 | ||
* Rad Eye GX, HP-4045 | * Rad Eye GX, HP-4045 | ||
* Ludlum Model 3000, HP-3166 Area Radiation Monitors and Continuous Air Monitors | * Ludlum Model 3000, HP-3166 | ||
Area Radiation Monitors and Continuous Air Monitors | |||
* 2-RE-6253 | * 2-RE-6253 | ||
* 2-RE-6259A | * 2-RE-6259A | ||
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* X-RE-5895B | * X-RE-5895B | ||
* 1-RE-6256 | * 1-RE-6256 | ||
* 1-RE-6295 Personnel Contamination Monitors, Portal Monitors and Small Article Monitors | * 1-RE-6295 | ||
Personnel Contamination Monitors, Portal Monitors and Small Article Monitors | |||
* SAM, HP-0063 | * SAM, HP-0063 | ||
* GEM-5, HP-0075 | * GEM-5, HP-0075 | ||
* SAM, HP-0055 | * SAM, HP-0055 | ||
* GEM-5, HP-0076 | * GEM-5, HP-0076 | ||
===Calibration and Testing Program (IP Section 02.02) (1 Sample)=== | ===Calibration and Testing Program (IP Section 02.02) (1 Sample)=== | ||
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: (1) Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors, Portal Monitors and Small Article Monitors | : (1) Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors, Portal Monitors and Small Article Monitors | ||
* GEM-5, HP-0075 | * GEM-5, HP-0075 | ||
* SAM, HP-0063 Failure to Meet Calibration or Source Check Acceptance Criteria | * SAM, HP-0063 | ||
Failure to Meet Calibration or Source Check Acceptance Criteria | |||
* Telepole, HP-1907 | * Telepole, HP-1907 | ||
* ARGOS, HP-0065 | * ARGOS, HP-0065 | ||
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* AMS-4, HP-2166 | * AMS-4, HP-2166 | ||
==71124.06 - Radioactive Gaseous and Liquid Effluent Treatment Walk Downs and Observations (IP Section 02.01) == | ==71124.06 - Radioactive Gaseous and Liquid Effluent Treatment== | ||
===Walk Downs and Observations (IP Section 02.01) (1 Sample)=== | |||
The inspectors walked down the following gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design: | |||
(1) | |||
* Plant Vent Stack Radiation Monitoring System | * Plant Vent Stack Radiation Monitoring System | ||
* Liquid Waste Processing Radiation Monitoring System | * Liquid Waste Processing Radiation Monitoring System | ||
* Turbine Sump Radiation Monitoring System | * Turbine Sump Radiation Monitoring System | ||
* Station Service Water to Discharge Canal Radiation Monitoring System Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample) | * Station Service Water to Discharge Canal Radiation Monitoring System Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample) | ||
The inspectors reviewed the following gaseous and liquid effluent monitor instrument calibrations and tests: | |||
The inspectors reviewed the following gaseous and liquid effluent monitor instrument calibrations and tests: | |||
(1) | |||
* WO 5360001, X-RE-5567A, South Plant Vent Stack Radiation Monitor Calibration, 07/30/2018 | * WO 5360001, X-RE-5567A, South Plant Vent Stack Radiation Monitor Calibration, 07/30/2018 | ||
* WO 5590739, X-RE-5570B, North Plant Vent Stack WRGM Radiation Monitor Calibration, 10/01/2019 | * WO 5590739, X-RE-5570B, North Plant Vent Stack WRGM Radiation Monitor Calibration, 10/01/2019 | ||
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* WO 5631300, 1-RE-4270, Unit 1 Station Service Water Train B to Discharge Canal Radiation Monitor Calibration, 01/14/2020 | * WO 5631300, 1-RE-4270, Unit 1 Station Service Water Train B to Discharge Canal Radiation Monitor Calibration, 01/14/2020 | ||
* WO 5576336, 2-RE-4269, Unit 2 Station Service Water Train A to Discharge Canal Radiation Monitor Calibration, 09/25/2019 | * WO 5576336, 2-RE-4269, Unit 2 Station Service Water Train A to Discharge Canal Radiation Monitor Calibration, 09/25/2019 | ||
* WO 5447947, X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System Flow Transmitter Calibration, 09/27/2018 | * WO 5447947, X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System Flow Transmitter Calibration, 09/27/2018 | ||
===Sampling and Analysis (IP Section 02.03) (1 Sample)=== | ===Sampling and Analysis (IP Section 02.03) (1 Sample)=== | ||
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: (1) Radioactive Effluent Sampling and Analysis Activities | : (1) Radioactive Effluent Sampling and Analysis Activities | ||
* Plant Ventilation Weekly Sampling, 01/27/2020 | * Plant Ventilation Weekly Sampling, 01/27/2020 | ||
* Containment Ventilation Sampling, 01/30/2020 Effluent Discharge Permits | * Containment Ventilation Sampling, 01/30/2020 | ||
Effluent Discharge Permits | |||
* G2018-034, Unit 1 Containment Vent, 02/27/2018 | * G2018-034, Unit 1 Containment Vent, 02/27/2018 | ||
* G2018-208, Plant Vent Stack B, 12/09/2018 | * G2018-208, Plant Vent Stack B, 12/09/2018 | ||
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* L2019-016, Plant Effluent Tank 1, 02/14/2019 | * L2019-016, Plant Effluent Tank 1, 02/14/2019 | ||
* L2019-055, Squaw Creek Reservoir, 08/01/2019 | * L2019-055, Squaw Creek Reservoir, 08/01/2019 | ||
* L2019-072, Plant Effluent Tank 2, 12/12/2019 | * L2019-072, Plant Effluent Tank 2, 12/12/2019 | ||
===Instrumentation and Equipment (IP Section 02.04) (1 Sample)=== | ===Instrumentation and Equipment (IP Section 02.04) (1 Sample)=== | ||
The inspectors reviewed the following radioactive effluent discharge system surveillance test results: | The inspectors reviewed the following radioactive effluent discharge system surveillance test results: | ||
(1) | (1) | ||
* WO 5319196, Primary Plant Ventilation Exhaust Filter Unit X-16 - Carbon Analysis B Train, 01/13/2018 | * WO 5319196, Primary Plant Ventilation Exhaust Filter Unit X-16 - Carbon Analysis B Train, 01/13/2018 | ||
* WO 5377734, Primary Plant Ventilation Exhaust Filter Unit X-01 - ESF Filter Test A Train, 10/31/2018 | * WO 5377734, Primary Plant Ventilation Exhaust Filter Unit X-01 - ESF Filter Test A Train, 10/31/2018 | ||
* WO 5431297, Primary Plant Ventilation Exhaust Filter Unit X-02 - ESF Filter Test B Train, 11/07/2018 | * WO 5431297, Primary Plant Ventilation Exhaust Filter Unit X-02 - ESF Filter Test B Train, 11/07/2018 | ||
* WO 5558463, Primary Plant Ventilation Exhaust Filter Unit X-02 - Carbon | * WO 5558463, Primary Plant Ventilation Exhaust Filter Unit X-02 - Carbon Analysis B Train, 09/18/2019 | ||
=== | ===Dose Calculations (IP Section 02.05) (1 Sample)=== | ||
The inspectors reviewed the following to asses public dose: | The inspectors reviewed the following to asses public dose: | ||
: (1) Liquid and Gaseous Discharge Permits | : (1) Liquid and Gaseous Discharge Permits | ||
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* L2019-016, Plant Effluent Tank 1, 02/14/2019 | * L2019-016, Plant Effluent Tank 1, 02/14/2019 | ||
* L2019-055, Squaw Creek Reservoir, 08/01/2019 | * L2019-055, Squaw Creek Reservoir, 08/01/2019 | ||
* L2019-072, Plant Effluent Tank 2, 12/12/2019 Annual Radiological Effluent Release Reports | * L2019-072, Plant Effluent Tank 2, 12/12/2019 | ||
Annual Radiological Effluent Release Reports | |||
* 2017 Annual Radioactive Effluent Release Report, 03/12/2018 | * 2017 Annual Radioactive Effluent Release Report, 03/12/2018 | ||
* 2018 Annual Radioactive Effluent Release Report, 04/20/2019 Abnormal Gaseous or Liquid Tank Discharges | * 2018 Annual Radioactive Effluent Release Report, 04/20/2019 | ||
Abnormal Gaseous or Liquid Tank Discharges | |||
* None were available for review during this inspection | * None were available for review during this inspection | ||
==71124.07 - Radiological Environmental Monitoring Program Site Inspection (IP Section 02.01) == | ==71124.07 - Radiological Environmental Monitoring Program== | ||
===Site Inspection (IP Section 02.01) (1 Sample)=== | |||
The inspectors evaluated the radiological environmental monitoring program implementation. | |||
: (1) The inspectors reviewed the following: | |||
Walkdowns, Calibrations, and Maintenance Record Review | Walkdowns, Calibrations, and Maintenance Record Review | ||
* Air sampling stations: A1, A2, A3, A4, A5, A6, A7, A8 | * Air sampling stations: A1, A2, A3, A4, A5, A6, A7, A8 | ||
| Line 272: | Line 322: | ||
* Air charcoal (A1, A2, A3, A4, A5, A6, A7, A8) | * Air charcoal (A1, A2, A3, A4, A5, A6, A7, A8) | ||
* Broad leaf (BL1, BL2, BL3) | * Broad leaf (BL1, BL2, BL3) | ||
* Surface water (SW1, SW2, SW3, SW4, SW5) | * Surface water (SW1, SW2, SW3, SW4, SW5) | ||
Licensee Actions in Response to Missed Sample, Inoperable Sampler, Lost Thermoluminescent Dosimeter (TLD) or Anomalous Measurement The inspectors reviewed the licensee's response to 13 missing or anomalous TLD results. The inspectors reviewed 6 inoperable samplers as noted in corrective action documents since May 2017 and noted in the 2017 and 2018 Annual Environmental Operating Reports. The majority of inoperable samplers were attributed to loss of power due to external events, such as weather and power line work. | |||
Licensee Actions in Response to Missed Sample, Inoperable Sampler, Lost Thermoluminescent Dosimeter (TLD) or Anomalous Measurement | |||
The inspectors reviewed the licensee's response to 13 missing or anomalous TLD results. The inspectors reviewed 6 inoperable samplers as noted in corrective action documents since May 2017 and noted in the 2017 and 2018 Annual Environmental Operating Reports. The majority of inoperable samplers were attributed to loss of power due to external events, such as weather and power line work. | |||
Sampling Program for the Potential of Licensed Material Entering Groundwater | Sampling Program for the Potential of Licensed Material Entering Groundwater | ||
* Groundwater Monitoring Wells: 9, 10, 11, 12, 14, 15, 16, 19, 25, CP-A, CP-B, CP-C | * Groundwater Monitoring Wells: 9, 10, 11, 12, 14, 15, 16, 19, 25, CP-A, CP-B, CP-C | ||
===Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)=== | ===Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)=== | ||
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==OTHER ACTIVITIES - BASELINE== | ==OTHER ACTIVITIES - BASELINE== | ||
===71151 - Performance Indicator Verification | |||
The inspectors verified licensee performance indicators submittals listed below: | |||
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)=== | |||
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) === | |||
{{IP sample|IP=IP 71151|count=2}} | {{IP sample|IP=IP 71151|count=2}} | ||
: (1) Unit 1 January 1, 2019, to December 31, 2019 | : (1) Unit 1 January 1, 2019, to December 31, 2019 | ||
: (2) Unit 2 January 1, 2019, to December 31 2019 IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) | : (2) Unit 2 January 1, 2019, to December 31 2019 | ||
(2 Samples) | |||
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples) | |||
: (1) Unit 1 January 1, 2019, to December 31, 2019 | : (1) Unit 1 January 1, 2019, to December 31, 2019 | ||
: (2) Unit 2 January 1, 2019, to December 31, 2019 | : (2) Unit 2 January 1, 2019, to December 31, 2019 | ||
===IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)=== | ===IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)=== | ||
: (1) Unit 1 January 1, 2019, to December 31, 2019 | : (1) Unit 1 January 1, 2019, to December 31, 2019 | ||
: (2) Unit 2 January 1, 2019, to December 31, 2019 | : (2) Unit 2 January 1, 2019, to December 31, 2019 | ||
===71153 - Follow-up of Events and Notices of Enforcement Discretion | |||
Event Follow-up (IP Section 03.01)=== | |||
{{IP sample|IP=IP 71153|count=1}} | {{IP sample|IP=IP 71153|count=1}} | ||
: (1) The inspectors evaluated licensee response to a Unit 2 reactor trip on January 1, 2020. | : (1) The inspectors evaluated licensee response to a Unit 2 reactor trip on January 1, 2020. | ||
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==INSPECTION RESULTS== | ==INSPECTION RESULTS== | ||
Manual Reactor Trip Due to Loss of both Main Feed Pumps Cornerstone | Manual Reactor Trip Due to Loss of both Main Feed Pumps Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events | ||
Green NCV 05000446/2020001-01 Open/Closed | |||
[H.12] - Avoid Complacency 71153 A self-revealed finding and associated non-cited violation (NCV) of very low safety significance occurred when the licensee failed to implement procedures for operation of the feed and condensate system as required by Technical Specification 5.4.1a. Specifically, while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the licensee isolated circulating water flow to the condensers, causing a loss of both Unit 2 main feedwater pumps. Control room operators manually insert a plant trip in response to the loss of feedwater. | |||
=====Description:===== | =====Description:===== | ||
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Corrective Actions: As an immediate corrective action, Comanche Peak operators tripped the Unit 2 reactor and stabilized the plant in mode 3. Personnel involved were removed from on-shift duties pending remedial training. Longer term actions included additional oversite of operations activities. Additional actions are discussed on AR 2020-00008. | Corrective Actions: As an immediate corrective action, Comanche Peak operators tripped the Unit 2 reactor and stabilized the plant in mode 3. Personnel involved were removed from on-shift duties pending remedial training. Longer term actions included additional oversite of operations activities. Additional actions are discussed on AR 2020-00008. | ||
Corrective Action References: CR-2020-00008 | Corrective Action References: CR-2020-00008 | ||
=====Performance Assessment:===== | =====Performance Assessment:===== | ||
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Violation: Technical Specification Section 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. NRC Regulatory Guide 1.33, Revision 2, Appendix A, Section 3, addresses Procedures for Startup, Operation, and Shutdown or Safety-Related PWR Systems and Section 3.K, addresses Feedwater System. The licensee established Procedure SOP-310B, Circulating Water, Revision 18, to address operation of the circulating water system, including adjusting flow to the auxiliary condensers which support operation of main feedwater system. | Violation: Technical Specification Section 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. NRC Regulatory Guide 1.33, Revision 2, Appendix A, Section 3, addresses Procedures for Startup, Operation, and Shutdown or Safety-Related PWR Systems and Section 3.K, addresses Feedwater System. The licensee established Procedure SOP-310B, Circulating Water, Revision 18, to address operation of the circulating water system, including adjusting flow to the auxiliary condensers which support operation of main feedwater system. | ||
Procedure SOP-310B, Revision 18, step 5.3.7, requires operators to slowly adjust the auxiliary condenser differential pressure to between 1- and 10 feet H2O. Contrary to the above, on January 1, 2020, the licensee failed to slowly adjust the auxiliary condenser differential pressure and maintain it between 1- and 10 feet H2O when operators fully closed the valves, causing a condition (dual feedwater pump trips on low vacuum) that required a reactor trip. | Procedure SOP-310B, Revision 18, step 5.3.7, requires operators to slowly adjust the auxiliary condenser differential pressure to between 1-and 10 feet H2O. Contrary to the above, on January 1, 2020, the licensee failed to slowly adjust the auxiliary condenser differential pressure and maintain it between 1-and 10 feet H2O when operators fully closed the valves, causing a condition (dual feedwater pump trips on low vacuum) that required a reactor trip. | ||
Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. | Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy. | ||
| Line 366: | Line 428: | ||
=DOCUMENTS REVIEWED= | =DOCUMENTS REVIEWED= | ||
Inspection Type | Inspection | ||
Procedure | |||
71111.04 | Type | ||
71111.05 | Designation | ||
Miscellaneous | Description or Title | ||
Drill 20-15-01 Fire Drill Scenario for EDG 2-02 810' Fuel Oil Transfer Pit March 3, | Revision or | ||
Date | |||
71111.04 | |||
Procedures | |||
SOP-103B | |||
Chemical and Volume Control System | |||
71111.05 | |||
Fire Plans | |||
FPI-105B | |||
U-2, train B Diesel generator and Equipment Elevation, 810' | |||
Miscellaneous | |||
Fire Hazard Analysis Report Sections 5.9.7 and 5.6 | |||
Drill 20-15-01 | |||
Fire Drill Scenario for EDG 2-02 810' Fuel Oil Transfer Pit | |||
March 3, | |||
20 | 20 | ||
71111.12 | 71111.12 | ||
Corrective Action | |||
Documents | Documents | ||
Miscellaneous | TR-YYYY-NNNN | ||
2016-008019 | |||
Miscellaneous | |||
Maintenance Rule Summary Report for Unit 1 and Unit 2 | |||
Auxiliary Feedwater | Auxiliary Feedwater | ||
Auxiliary Feedwater System Status | 2/18/2020 | ||
Auxiliary Feedwater System Status | |||
2nd Quarter | |||
FY19 | FY19 | ||
71111.13 | 71111.13 | ||
Miscellaneous | Drawings | ||
E2-0026 | |||
6.9KV Three Line Diagram Normal Buses | |||
Miscellaneous | |||
STI-600.01-1 | |||
Guarded Equipment Management Posting Log | |||
February 12, | |||
20 | 20 | ||
Procedures | Procedures | ||
Work Orders | SOP-310B | ||
71111.15 | Circulating water System | ||
Work Orders | |||
5835726 | |||
Auxiliary Feedwater Pump Turbine 2-01Govenor Stroke | |||
2/13/2020 | |||
71111.15 | |||
Corrective Action | |||
Documents | |||
CR | |||
2019-9530 | |||
2/13/2019 | |||
TR | |||
20-1247 | |||
February 19, | |||
20 | 20 | ||
Drawings | Drawings | ||
Operability | M2-2760 | ||
Diesel Engine Start/Stop Logic | |||
CR- | Operability | ||
71111.19 | Evaluations | ||
FSAR Table 8.3-1, Loading Requirements for Loss of | |||
Coolant Accident Coincident with Loss of Offsite Power | |||
104 | |||
CR- | |||
20-001295 | |||
71111.19 | |||
Corrective Action | |||
Documents | |||
CR-YYYY-NNNN | |||
2019-009453 | |||
IR-2020-001597 | |||
Multiple Relays Out of Tolerance on Unit 2 Train B | |||
Sequencer | Sequencer | ||
Procedures | Procedures | ||
INC-7393A | |||
CH Cal Neutron Flux Power Range ION Current Gain and | |||
Summing Level Amplifier | Summing Level Amplifier | ||
MSE-S2-0673B | MSE-S2-0673B | ||
Work Orders | Unit 2 Train B Sequencer Under Voltage Relay Surveillance | ||
WO 5840776 | Work Orders | ||
documented in IR-2019-009453 | WO 5666818 | ||
Inspection Type | Perform MSE-S2-0673B, TR B Sequencer UV Relay | ||
WO 5840776 | |||
WO 5848383 | Troubleshoot and Repair Sequence Alarm Circuit as | ||
WO 5866715 | documented in IR-2019-009453 | ||
WO 5866789 | |||
Inspection | |||
Procedure | |||
Type | |||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
WO 5848383 | |||
Replace Cell 22 on BT1D4 at Power | |||
WO 5866715 | |||
Perform CCAL IAW INC-7393A | |||
WO 5866789 | |||
Troubleshoot test signal going to zero described in CR 2020- | |||
001447 | 001447 | ||
71111.20 | 71111.20 | ||
Miscellaneous | |||
BEACON 3D Reactivity Projection for Unit 2 Forced Outage | |||
Startup | Startup | ||
71111.22 | 01/01/2020 | ||
OPT-106A | 71111.22 | ||
OPT-467A | Procedures | ||
Work Orders | ETP-106 | ||
Monthly RCCA Repositioning | |||
OPT-106A | |||
Control Rod Exercise | |||
OPT-467A | |||
Train A Safeguards Slave relay K609 Actuation Test | |||
Revision 5 | |||
Work Orders | |||
WO 5656218 | |||
Solid State Protection System Slave Relay Test | |||
March 11, | |||
20 | 20 | ||
WO 5659452 | WO 5659452 | ||
WO 5829754 | Perform NUC 202 AT-Power MTC Measurement | ||
WO 5846000 | WO 5829754 | ||
WO 5852752 | OPT-106A, Control Rod Exercise Test | ||
71114.06 | WO 5846000 | ||
Monthly RCCA Repost ETP-106 | |||
WO 5852752 | |||
IR-2020-000542 Troubleshoot 2-01 EDG Volt Reg TRBL | |||
71114.06 | |||
Miscellaneous | |||
ERO team Exercise | |||
February 9, | |||
20 | 20 | ||
71124.05 | 71124.05 | ||
Calibration | |||
391556 | Records | ||
4373552 | 3443188 | ||
4374577 | X-RE-5700 ICI-4998, CCAL FB VNT EXH | ||
26655 | 06/24/2009 | ||
20934 | 3648653 | ||
5371788 | 2-RE-6297, ICI-4961 Channel Calibration | ||
22342 | 09/30/2010 | ||
22458 | 391556 | ||
26341 | 1-RE-6295 ICI-4961, CCAL | ||
ASCAN | 03/16/2009 | ||
FSCAN | 4373552 | ||
HP-0058 | 1-RE-6295 ICI-4961, CCAL | ||
HP-0063 | 04/12/2016 | ||
HP-0075 | 4374577 | ||
Inspection Type | 2-RE-6297 ICI-4961, CCAL | ||
05/10/2017 | |||
HP-1206 | 26655 | ||
HP-2166 | X-RE-5700 ICI-4998, CCAL FB VNT EXH | ||
HP-4124 | 01/22/2015 | ||
HP-5002 | 20934 | ||
HP-711812 | 1-RE-6256 ICI-4959 CCAL HRAM | ||
Corrective Action CR-YYYY-NNNN | 06/09/2015 | ||
5371788 | |||
X-RE-5701 INC-4915X, CCAL AB VNT GPRM | |||
07/18/2019 | |||
22342 | |||
1-RE-6290A INC-7079, CCAL CNTMT HRRM | |||
05/16/2019 | |||
22458 | |||
1-RE-6290B INC-7079, CCAL CNTMT HRRM | |||
05/02/2019 | |||
26341 | |||
1-RUK-2326A/2328A INC-4916 CCAL | |||
07/17/2019 | |||
ASCAN | |||
WBC System Calibration Data Package | |||
11/20/2019 | |||
FSCAN | |||
WBC System Calibration Data Package | |||
09/12/2019 | |||
HP-0058 | |||
Argos/Sirius Calibration Data Sheet | |||
11/10/2019 | |||
HP-0063 | |||
NE Technology SAM Calibration Data Sheet | |||
10/22/2018 | |||
HP-0075 | |||
GEM-5 Calibration Data Sheet | |||
2/04/2019 | |||
Inspection | |||
Procedure | |||
Type | |||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
HP-1206 | |||
Ludlum Model 177 Frisker Calibration Data Sheet | |||
01/27/2020 | |||
HP-2166 | |||
AMS-4 Calibration Data Sheet | |||
10/04/2019 | |||
HP-4124 | |||
Thermo RO-20AA Calibration Data Sheet | |||
01/29/2020 | |||
HP-5002 | |||
Low Volume Air Sampler Calibration Data Sheet | |||
10/12/2018 | |||
HP-711812 | |||
RDS-31 Calibration Data Sheet | |||
10/07/2019 | |||
Corrective Action | |||
Documents | |||
CR-YYYY-NNNN | |||
2011-006222, 2016-001350, 2018-003694, 2018-006522, | |||
2018-006631, 2018-007217, 2019-000184, 2019-001550, | |||
2019-004125, 2019-004570, 2019-005318, 2019-007716, | 2019-004125, 2019-004570, 2019-005318, 2019-007716, | ||
2019-008045, 2019-008114, 2019-008129 | 2019-008045, 2019-008114, 2019-008129 | ||
TR-YYYY-NNNN | TR-YYYY-NNNN | ||
2018-006999, 2018-007197, 2018-007846, 2019-001511, | |||
2019-003201, 2019-003405, 2019-003992, 2019-004146, | 2019-003201, 2019-003405, 2019-003992, 2019-004146, | ||
2019-004149, 2019-004221, 2019-005656, 2020-000063 | 2019-004149, 2019-004221, 2019-005656, 2020-000063 | ||
Corrective Action | Corrective Action | ||
Documents | Documents | ||
Resulting from | Resulting from | ||
Inspection | Inspection | ||
Miscellaneous | CR-YYYY-NNNN | ||
19-001 through | 20-000750, 2020-000783, 2020-000814 | ||
Miscellaneous | |||
1-RE-6290A | |||
Last Detector Primary Calibration | |||
05/15/2019 | |||
19-001 through | |||
19-007 | 19-007 | ||
2Qtr FY19 | Calibration Well Source Charts | ||
T190990 | 08/08/2019 | ||
Procedures | 2Qtr FY19 | ||
ICI-4959 | CPNPP System Status: Radiation Monitoring | ||
ICI-4961 | T190990 | ||
ICI-4998 | RadCal 2026C and 1800cc, 180cc, and 6cc detectors | ||
INC-7079 | 05/29/2019 | ||
Procedures | |||
CLI-782 | |||
APEX Gamma Spectroscopy Counting System | |||
ICI-4959 | |||
Channel Calibration - High Range Area Radiation Monitors | |||
ICI-4961 | |||
Channel Calibration - Digital High Range Area Monitors | |||
ICI-4998 | |||
Channel Calibration - Gas Process Radiation Monitor | |||
INC-7079 | |||
Channel Calibration - | |||
Containment High Range Radiation Monitor Channels | Containment High Range Radiation Monitor Channels | ||
1-RE-6290A/B and 2-RE-6290A/B | 1-RE-6290A/B and 2-RE-6290A/B | ||
RPI-301 | |||
RPI-800 | RPI-301 | ||
RPI-802 | Portable Survey Instruments | ||
RPI-862 | RPI-800 | ||
Control of Radiation Protection Equipment | |||
RPI-802 | |||
Performance of Source Checks | |||
RPI-862 | |||
Calibration of the Argos/Sirius Personnel Contamination | |||
Monitor and Gem-5 Gamma Exit Monitor | Monitor and Gem-5 Gamma Exit Monitor | ||
STA-619 | STA-619 | ||
Inspection Type | Administrative Control of Digital Radiation Monitoring System | ||
STA-650 | Inspection | ||
STA-658 | Procedure | ||
STA-677 | Type | ||
STA-700 | Designation | ||
STI-677.01 | Description or Title | ||
Self-Assessments | Revision or | ||
EVAL-2019-007 Chemistry Control and Chemistry Measurement & Analysis | Date | ||
71124.06 | STA-650 | ||
General Health Physics Plan | |||
WO 5421935 | STA-658 | ||
Radiation Protection Equipment Calibration Program | |||
STA-677 | |||
Preventative Maintenance Program | |||
STA-700 | |||
Surveillance Frequency Control Program | |||
STI-677.01 | |||
PM Change Processing | |||
Self-Assessments EVAL-2018-006 | |||
Work Management/Radiation Protection Audit | |||
08/02/2018 | |||
EVAL-2019-007 | |||
Chemistry Control and Chemistry Measurement & Analysis | |||
11/21/2019 | |||
71124.06 | |||
Calibration | |||
Records | |||
WO 5360001 | |||
X-RE-5567A, South Plant Vent Stack Radiation Monitor | |||
Calibration | |||
07/30/2018 | |||
WO 5421935 | |||
1-RE-4269, Unit 1 Station Service Water Train A to | |||
Discharge Canal Radiation Monitor Calibration | Discharge Canal Radiation Monitor Calibration | ||
WO 5447947 | 10/24/2018 | ||
WO 5447947 | |||
X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System | |||
Flow Transmitter Calibration | Flow Transmitter Calibration | ||
WO 5556086 | 09/27/2018 | ||
WO 5576336 | WO 5556086 | ||
2-RE-5100, Turbine Sump 2-04 Radiation Monitor Calibration 06/12/2019 | |||
WO 5576336 | |||
2-RE-4269, Unit 2 Station Service Water Train A to | |||
Discharge Canal Radiation Monitor Calibration | Discharge Canal Radiation Monitor Calibration | ||
WO 5585319 | 09/25/2019 | ||
WO 5585319 | |||
X-RE-5253, Liquid Waste Processing Discharge Radiation | |||
Monitor Calibration | Monitor Calibration | ||
WO 5590739 | 10/28/2019 | ||
WO 5590739 | |||
X-RE-5570B, North Plant Vent Stack WRGM Radiation | |||
Monitor Calibration | Monitor Calibration | ||
WO 5631300 | 10/01/2019 | ||
WO 5631300 | |||
1-RE-4270, Unit 1 Station Service Water Train B to | |||
Discharge Canal Radiation Monitor | Discharge Canal Radiation Monitor | ||
Corrective Action CR-YYYY-NNNN | 01/14/2020 | ||
Corrective Action | |||
Documents | |||
CR-YYYY-NNNN | |||
2019-008687, 2019-008794 | |||
TR-YYYY-NNNN | |||
2017-000757, 2018-003362, 2019-001642, 2019-005866, | |||
2019-006713, 2019-008605 | 2019-006713, 2019-008605 | ||
Corrective Action | Corrective Action | ||
Documents | Documents | ||
Resulting from | Resulting from | ||
Inspection | Inspection | ||
Miscellaneous | TR-YYYY-NNNN | ||
2017 Annual Radioactive Effluent Release Report | 20-000766, 2020-000815, 2020-000817 | ||
2018 Annual Radioactive Effluent Release Report | TR-YYYY-NNNN | ||
G2018-034 | 20-000766, 2020-000815, 2020-000817 | ||
G2018-208 | Miscellaneous | ||
Inspection Type | CPSES Offsite Dose Calculation Manual, Unit 1 and Unit 2 | ||
G2018-210 | 2017 Annual Radioactive Effluent Release Report | ||
G2019-046 | 03/12/2018 | ||
G2019-193 | 2018 Annual Radioactive Effluent Release Report | ||
G2019-216 | 04/20/2019 | ||
L2018-023 | G2018-034 | ||
L2018-040 | Gaseous Discharge Permit - Unit 1 Containment Vent | ||
L2018-051 | 2/27/2018 | ||
L2019-016 | G2018-208 | ||
L2019-055 | Gaseous Discharge Permit - Plant Vent Stack B | ||
L2019-072 | 2/09/2018 | ||
Procedures | |||
CHM-230 | Inspection | ||
CLI-744 | Procedure | ||
CLI-745 | Type | ||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
G2018-210 | |||
Gaseous Discharge Permit - Non-Routine Gas Normal | |||
2/10/2018 | |||
G2019-046 | |||
Gaseous Discharge Permit - Plant Vent Stack B | |||
03/12/2019 | |||
G2019-193 | |||
Gaseous Discharge Permit - Unit 2 Containment Vent | |||
11/24/2019 | |||
G2019-216 | |||
Gaseous Discharge Permit - Plant Vent Stack A | |||
2/31/2019 | |||
L2018-023 | |||
Liquid Discharge Permit - Plant Effluent Tank 1 | |||
07/05/2018 | |||
L2018-040 | |||
Liquid Discharge Permit - Plant Effluent Tank 2 | |||
10/24/2018 | |||
L2018-051 | |||
Liquid Discharge Permit - Low Volume Waste Pond (LVWP) | |||
2/01/2018 | |||
L2019-016 | |||
Liquid Discharge Permit - Plant Effluent Tank 1 | |||
2/14/2019 | |||
L2019-055 | |||
Liquid Discharge Permit - Squaw Creek Reservoir | |||
08/01/2019 | |||
L2019-072 | |||
Liquid Discharge Permit - Plant Effluent Tank 2 | |||
2/12/2019 | |||
Procedures | |||
CHM-170 | |||
Liquid and Gaseous Effluent Program | |||
CHM-230 | |||
Guidelines for Sample Collection | |||
CLI-744 | |||
Radioactive Effluent Pre-Release Permit Processing | |||
CLI-745 | |||
Radioactive Effluent Post-Release Permit Processing and | |||
Surveillance Tracking | Surveillance Tracking | ||
STA-603 | STA-603 | ||
STA-619 | Control of Station Radioactive Effluents | ||
STA-619 | |||
Administrative Control of the Digital Radiation Monitoring | |||
System | System | ||
STA-677 | STA-677 | ||
Self-Assessments | Preventive Maintenance Program | ||
Self-Assessments EVAL-2019-007 | |||
Radioactive Waste, Effluents, Environmental, and Chemistry | |||
Programs | Programs | ||
Work Orders | 11/21/2019 | ||
WO 5377734 | Work Orders | ||
WO 5431297 | WO 5319196 | ||
WO 5558463 | Primary Plant Ventilation Exhaust Filter Unit X-16 | ||
71124.07 | 01/31/2018 | ||
WO 5377734 | |||
TR-YYYY-NNNN | Primary Plant Ventilation Exhaust Filter Unit X-01 | ||
10/03/2018 | |||
WO 5431297 | |||
Primary Plant Ventilation Exhaust Filter Unit X-02 | |||
11/17/2018 | |||
WO 5558463 | |||
Primary Plant Ventilation Exhaust Filter Unit X-02 | |||
09/18/2019 | |||
71124.07 | |||
Corrective Action | |||
Documents | |||
CR-YYYY-NNNN | |||
2018-001574, 2018-001611, 2018-001760, 2018-004523, | |||
2019-002077 | |||
TR-YYYY-NNNN | |||
2018-001867, 2018-004228, 2019-001642, 2019-007287 | |||
2019-008284, 2019-009052, 2019-009165 | 2019-008284, 2019-009052, 2019-009165 | ||
Corrective Action | Corrective Action | ||
Documents | Documents | ||
Resulting from | Resulting from | ||
Inspection | Inspection | ||
Inspection Type | CR-YYYY-NNNN | ||
20-000748 | |||
Miscellaneous | |||
2018 Annual Radiological Environmental Operating Report | Inspection | ||
NUPIC Audit | Procedure | ||
Type | |||
Designation | |||
Description or Title | |||
Revision or | |||
Date | |||
Miscellaneous | |||
2017 Annual Radiological Environmental Operating Report | |||
04/30/2018 | |||
2018 Annual Radiological Environmental Operating Report | |||
04/01/2019 | |||
NUPIC Audit | |||
23724 | 23724 | ||
GEL Laboratories (JQA-14-097) | |||
24747 | 05/29/2014 | ||
NUPIC Audit | |||
ODCM | 24747 | ||
(NOV2019-069) | |||
GEL Laboratories (NOD-19-018) | |||
08/29/2019 | |||
ODCM | |||
Comanche Peak Steam Electric Station Offsite Dose | |||
Calculation Manual Unit 1 and Unit 2 | Calculation Manual Unit 1 and Unit 2 | ||
RPI-714-1- | RPI-714-1- | ||
20180715 | 20180715 | ||
RPI-714-1- | 2018 Land Use Census | ||
07/31/2018 | |||
RPI-714-1- | |||
20190620 | 20190620 | ||
Procedures | 2019 Land Use Census | ||
RPI-710 | 07/25/2019 | ||
Procedures | |||
RPI-538 | |||
Process Environmental Badges | |||
RPI-710 | |||
Radiological Environmental Monitoring, Sampling, and | |||
Analysis Program | Analysis Program | ||
RPI-713 | RPI-713 | ||
Collection, Preparation, and Shipment of Radiological | |||
Environmental Samples | Environmental Samples | ||
RPI-714 | RPI-714 | ||
RPI-888 | Land Use Census | ||
STA-653 | RPI-888 | ||
STA-654 | Calibration of Portable Air Sample Equipment | ||
Self-Assessments EVAL-2019-007 Radioactive Waste, Effluents, Environmental, and Chemistry | STA-653 | ||
Contamination Control Program | |||
STA-654 | |||
Groundwater Protection Program | |||
Self-Assessments EVAL-2019-007 | |||
Radioactive Waste, Effluents, Environmental, and Chemistry | |||
Programs | Programs | ||
Work Orders | 11/21/2019 | ||
Work Orders | |||
WO- | |||
4938991, 4965490, 5052258, 5080201, 5490927, | |||
5651858, 5654059, 5654081, 5654093, 5654106, | 5651858, 5654059, 5654081, 5654093, 5654106, | ||
5654119, 5654136, 5659602, 5659645, 5667801, | 5654119, 5654136, 5659602, 5659645, 5667801, | ||
5736155, 5736168, 5736197, 5736232, 5736248, | 5736155, 5736168, 5736197, 5736232, 5736248, | ||
5736282, 5736299, 5741625, 5747140 | 5736282, 5736299, 5741625, 5747140 | ||
}} | }} | ||
Latest revision as of 05:57, 16 March 2025
| ML20353A072 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 12/22/2020 |
| From: | O'Keefe N NRC Region 4 |
| To: | Peters K Vistra Operations Company |
| References | |
| IR 2020001 | |
| Download: ML20353A072 (24) | |
Text
December 22, 2020
SUBJECT:
REVISED REPORT - COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000445/2020001 AND 05000446/2020001
Dear Mr. Peters:
On March 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Comanche Peak Nuclear Power Plant, Units 1 and 2. On April 2, 2020, the NRC inspectors discussed the results of this inspection with Mr. T. McCool, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC is issuing this revision to the subject report to document inspection of a Unit 2 unplanned outage during the inspection period under Inspection Procedure, 71111.20 -
Refueling and Other Outage Activities, of the attached report. NRC Inspection Report 0500445/2020001 and 0500446/2020001 (ADAMS Accession No. ML20128J555) was initially issued on May 7, 2020, and this revised report replaces it entirely.
One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at Comanche Peak Nuclear Power Plant, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Neil F. O'Keefe, Chief Reactor Projects Branch B Division of Reactor Projects
Docket Nos. 05000445 and 05000446 License Nos. NPF-87 and NPF-89
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000445 and 05000446
License Numbers:
Report Numbers:
05000445/2020001 and 05000446/2020001
Enterprise Identifier: I-2020-001-0010
Licensee:
VISTRA Operations Company, LLC
Facility:
Comanche Peak Nuclear Power Plant, Units 1 and 2
Location:
Glen Rose, TX 76043
Inspection Dates:
January 1 to March 31, 2020
Inspectors:
J. Ellegood, Senior Resident Inspector
D. Antonangeli, Health Physicist
B. Baca, Health Physicist
N. Day, Resident Inspector
N. Greene, Senior Health Physicist
J. Melfi, Project Engineer
J. O'Donnell, Senior Health Physicist
Approved By:
Neil F. O'Keefe, Chief
Reactor Projects Branch B
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Comanche Peak Nuclear Power Plant,
Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Manual Reactor Trip Due to Loss of both Main Feed Pumps Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000446/2020001-01 Open/Closed
[H.12] - Avoid Complacency 71153 A self-revealed finding and associated non-cited violation (NCV) of very low safety significance occurred when the licensee failed to implement procedures for operation of the feed and condensate system as required by Technical Specification 5.4.1.a. Specifically, while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the operators isolated circulating water flow to the condensers, causing a loss of both Unit 2 main feedwater pumps. Control room operators manually insert a plant trip in response to the loss of feedwater.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000446/2018-002-01 LER 2018-002-01 for Comanche Peak, Unit 2,
Automatic Actuation of Auxiliary Feedwater System.
71153 Closed LER 05000446/2019-002-00 LER 2019-002-00 for Comanche Peak Nuclear Power Plant, Unit 2,
Automatic Actuation of Auxiliary Feedwater System.
71153 Closed
PLANT STATUS
Unit 1 began the inspection period at rated thermal power and remained there throughout the inspection period.
Unit 2 began the inspection period at rated thermal power. On January 1, 2020, the licensee inserted a manual trip in response to a loss of both main feed pumps while adjusting circulating water flow to the auxiliary condensers. The licensee took the reactor critical and synchronized to the grid on January 3, 2020. The licensee reached 100 percent power on January 4, 2020 and remained at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. From January 1 - March 19, 2020, the inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; and observed risk-significant activities when warranted. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In the cases where it was determined the objectives and requirements could not be performed remotely, management elected to postpone and reschedule the inspection to a later date.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from forecasted thunderstorms on January 10, 2020
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (1 Sample)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2, chemical and volume control system on February 6, 2020
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Unit 1, turbine building basement on January 17, 2020
- (2) Unit 2, turbine building basement on January 17, 2020
- (3) Unit 2, emergency diesel generator A room on January 23, 2020
- (4) Service water intake structure building on March 26, 2020
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill on March 3, 2020
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the control room during turbine start and synchronization to the grid on January 3, 2020
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated licensed operators for just in time training for a reactor startup on January 2, 2020
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
- (1) Unit 2, auxiliary feedwater system on February 25, 2020
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed;
- (1) Realignment of the Units 1 and 2 circulating water system on January 15, 2020
- (2) Planned yellow risk for Unit 1 auxiliary feedwater valve strokes concurrent with emergent work to restore the Unit 1 emergency diesel generator A to operable status on February 14, 2020
- (3) Risk associated with switchyard work and troubleshooting of Unit 2 circulating water pump on February 7, 2020
- (4) Risk associated with starting the Unit 2 circulating water pump 2 on March 5, 2020
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) Unit 1, residual heat removal systems A and B, due to increasing pressures as described in condition report CR-2019-009779 on January 9, 2020
- (2) Unit 2, emergency diesel generator A, due to a degraded time delay device as described in condition report CR-2020-001295 on February 24, 2020
- (3) Unit 2, safety chiller 2-06, tripping due to a shorting bulb socket assembly as described in condition report CR 2020-001502 on March 2, 2020
- (4) Unit 2, control rods from potential thermal sleeve cracking as described in Part 21 report LTR-NRC-19-79, and corrective action document TR 2020-1247
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the following post maintenance test activities to verify system operability and functionality:
- (1) Repair of disconnected wires and replacement of components in the Unit 2 safeguard sequencer system per Work Order 5840776 on February 20, 2020
- (2) Replacement of cell 22 on battery 1DT4 per Work Order 5848383 on January 31, 2020
- (3) Repair of failed switch on neutron flux power ranch channel N-42 per Work Order 5866789 on February 28, 2020
- (4) As found testing, calibration, and installation of Unit 2 safeguard sequencer B undervoltage relays per Work Order 5666818 on March 4, 2020.
71111.20 - Refueling and Other Outage Activities
Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated licensee activities during a Unit 2 unplanned outage from January 1-3, 2020.
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01)
- (1) Unit 2, emergency diesel generator monthly load test per Procedure OPT 214B, Diesel Generator Operability Test, Revision 16, on January 22, 2020
- (2) Unit 2, at power end of core life reactivity test per Work Order 5659452 on February 10, 2020
- (3) Unit 1, monthly control rod exercise surveillance per Work Order 5829754 on January 24, 2020
- (4) Unit 1, train A slave relay K609 actuation test per Work Order 5656218 on March 11, 2020
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
- (1) The blue team emergency preparedness drill on February 19,
RADIATION SAFETY
71124.05 - Radiation Monitoring Instrumentation
Walk Downs and Observations (IP Section 02.01) (1 Sample)
The inspectors evaluated the following radiation detection instrumentation during plant walkdowns:
- (1) Portable Survey Instruments
- RM-177, HP-1461
- RM-177, HP-1113
- RM-177, HP-1145
- RM-177, HP-2400
- RM-177, HP-1464
- RM-177, HP-1081
- RM-177, HP-1026
- AMS-4, HP-2166
- 3030E, HP-3270
Source Check Demonstration
- Rad Eye G, HP-3112
- Telepole, HP-1906
- Rad Eye GX, HP-4045
- Ludlum Model 3000, HP-3166
Area Radiation Monitors and Continuous Air Monitors
- 2-RE-6253
- 2-RE-6259A
- 2-RE-6297
- X-RE-5896A
- X-RE-5895B
- 1-RE-6256
- 1-RE-6295
Personnel Contamination Monitors, Portal Monitors and Small Article Monitors
- SAM, HP-0063
- GEM-5, HP-0075
- SAM, HP-0055
- GEM-5, HP-0076
Calibration and Testing Program (IP Section 02.02) (1 Sample)
The inspectors evaluated the calibration and testing of the following radiation detection instruments:
- (1) Alarm Setpoint and Calibration Method Check of Personnel Contamination Monitors, Portal Monitors and Small Article Monitors
- GEM-5, HP-0075
- SAM, HP-0063
Failure to Meet Calibration or Source Check Acceptance Criteria
- Telepole, HP-1907
- ARGOS, HP-0065
- RO-20AA, HP-4123
- AMS-4, HP-2166
71124.06 - Radioactive Gaseous and Liquid Effluent Treatment
Walk Downs and Observations (IP Section 02.01) (1 Sample)
The inspectors walked down the following gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design:
(1)
- Plant Vent Stack Radiation Monitoring System
- Liquid Waste Processing Radiation Monitoring System
- Turbine Sump Radiation Monitoring System
- Station Service Water to Discharge Canal Radiation Monitoring System Calibration and Testing Program (Process & Effluent Monitors) (IP Section 02.02) (1 Sample)
The inspectors reviewed the following gaseous and liquid effluent monitor instrument calibrations and tests:
(1)
- WO 5360001, X-RE-5567A, South Plant Vent Stack Radiation Monitor Calibration, 07/30/2018
- WO 5590739, X-RE-5570B, North Plant Vent Stack WRGM Radiation Monitor Calibration, 10/01/2019
- WO 5585319, X-RE-5253, Liquid Waste Processing Discharge Radiation Monitor Calibration, 10/28/2019
- WO 5556086, 2-RE-5100, Turbine Sump 2-04 Radiation Monitor Calibration, 06/12/2019
- WO 5421935, 1-RE-4269, Unit 1 Station Service Water Train A to Discharge Canal Radiation Monitor Calibration, 10/24/2018
- WO 5631300, 1-RE-4270, Unit 1 Station Service Water Train B to Discharge Canal Radiation Monitor Calibration, 01/14/2020
- WO 5576336, 2-RE-4269, Unit 2 Station Service Water Train A to Discharge Canal Radiation Monitor Calibration, 09/25/2019
- WO 5447947, X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System Flow Transmitter Calibration, 09/27/2018
Sampling and Analysis (IP Section 02.03) (1 Sample)
The inspectors reviewed the following:
- (1) Radioactive Effluent Sampling and Analysis Activities
- Plant Ventilation Weekly Sampling, 01/27/2020
- Containment Ventilation Sampling, 01/30/2020
Effluent Discharge Permits
- G2018-034, Unit 1 Containment Vent, 02/27/2018
- G2018-208, Plant Vent Stack B, 12/09/2018
- G2018-210, Non-Routine Gas Normal, 12/10/2018
- G2019-046, Plant Vent Stack B, 03/12/2019
- G2019-193, Unit 2 Containment Vent, 11/24/2019
- G2019-216, Plant Vent Stack A, 12/31/2019
- L2018-023, Plant Effluent Tank 1, 07/05/2018
- L2018-040, Plant Effluent Tank 2, 10/24/2018
- L2018-051, Low Volume Waste Pond (LVWP), 12/01/2018
- L2019-016, Plant Effluent Tank 1, 02/14/2019
- L2019-055, Squaw Creek Reservoir, 08/01/2019
- L2019-072, Plant Effluent Tank 2, 12/12/2019
Instrumentation and Equipment (IP Section 02.04) (1 Sample)
The inspectors reviewed the following radioactive effluent discharge system surveillance test results:
(1)
- WO 5319196, Primary Plant Ventilation Exhaust Filter Unit X-16 - Carbon Analysis B Train, 01/13/2018
- WO 5377734, Primary Plant Ventilation Exhaust Filter Unit X-01 - ESF Filter Test A Train, 10/31/2018
- WO 5431297, Primary Plant Ventilation Exhaust Filter Unit X-02 - ESF Filter Test B Train, 11/07/2018
- WO 5558463, Primary Plant Ventilation Exhaust Filter Unit X-02 - Carbon Analysis B Train, 09/18/2019
Dose Calculations (IP Section 02.05) (1 Sample)
The inspectors reviewed the following to asses public dose:
- (1) Liquid and Gaseous Discharge Permits
- G2018-034, Unit 1 Containment Vent, 02/27/2018
- G2018-208, Plant Vent Stack B, 12/09/2018
- G2018-210, Non-Routine Gas Normal, 12/10/2018
- G2019-046, Plant Vent Stack B, 03/12/2019
- G2019-193, Unit 2 Containment Vent, 11/24/2019
- G2019-216, Plant Vent Stack A, 12/31/2019
- L2018-023, Plant Effluent Tank 1, 07/05/2018
- L2018-040, Plant Effluent Tank 2, 10/24/2018
- L2018-051, Low Volume Waste Pond (LVWP), 12/01/2018
- L2019-016, Plant Effluent Tank 1, 02/14/2019
- L2019-055, Squaw Creek Reservoir, 08/01/2019
- L2019-072, Plant Effluent Tank 2, 12/12/2019
Annual Radiological Effluent Release Reports
- 2017 Annual Radioactive Effluent Release Report, 03/12/2018
- 2018 Annual Radioactive Effluent Release Report, 04/20/2019
Abnormal Gaseous or Liquid Tank Discharges
- None were available for review during this inspection
71124.07 - Radiological Environmental Monitoring Program
Site Inspection (IP Section 02.01) (1 Sample)
The inspectors evaluated the radiological environmental monitoring program implementation.
- (1) The inspectors reviewed the following:
Walkdowns, Calibrations, and Maintenance Record Review
- Air sampling stations: A1, A2, A3, A4, A5, A6, A7, A8
- Thermoluminescent dosimeter (TLD) monitoring stations: R1, R4, R11, R13, R22, R25, R27, R29, R30, R36
- Calibrations of selected air sample pumps: 2178, 2196B, 2214, and 2224 Environmental Sample Collections and Preparation Observation
- Air particulate (A1, A2, A3, A4, A5, A6, A7, A8)
- Air charcoal (A1, A2, A3, A4, A5, A6, A7, A8)
- Broad leaf (BL1, BL2, BL3)
- Surface water (SW1, SW2, SW3, SW4, SW5)
Licensee Actions in Response to Missed Sample, Inoperable Sampler, Lost Thermoluminescent Dosimeter (TLD) or Anomalous Measurement
The inspectors reviewed the licensee's response to 13 missing or anomalous TLD results. The inspectors reviewed 6 inoperable samplers as noted in corrective action documents since May 2017 and noted in the 2017 and 2018 Annual Environmental Operating Reports. The majority of inoperable samplers were attributed to loss of power due to external events, such as weather and power line work.
Sampling Program for the Potential of Licensed Material Entering Groundwater
Groundwater Protection Initiative (GPI) Implementation (IP Section 02.02) (1 Sample)
- (1) The inspectors evaluated the licensee's voluntary groundwater protection initiative.
A few observations were as follows:
- The general maintenance and material condition of the groundwater monitoring wells was adequate with the general area around the well was kept clear of any obstructions.
- Most monitoring wells had enough water for samples to be taken.
- Monitoring well locations 11 and CP-A had results of 835 and 1700 pCi/L, respectively, which are both below their lower limit of detection (LLD)requirements. The remaining well location samples all tested below the minimum detectable activity.
- The licensee implemented additional surface water sampling of the drainage flow catch basin to track the potential impact of a water treatment filtered water storage tank leak. The licensee has corrective actions in progress to address the identified leak.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===
- (1) Unit 1 January 1, 2019, to December 31, 2019
- (2) Unit 2 January 1, 2019, to December 31 2019
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)
- (1) Unit 1 January 1, 2019, to December 31, 2019
- (2) Unit 2 January 1, 2019, to December 31, 2019
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)
- (1) Unit 1 January 1, 2019, to December 31, 2019
- (2) Unit 2 January 1, 2019, to December 31, 2019
===71153 - Follow-up of Events and Notices of Enforcement Discretion
Event Follow-up (IP Section 03.01)===
- (1) The inspectors evaluated licensee response to a Unit 2 reactor trip on January 1, 2020.
Event Report (IP Section 03.02) (2 Samples)
The inspectors evaluated the following licensee event reports (LERs):
- (1) LER 05000446/2019-002-00, Automatic Actuation of Auxiliary Feedwater System (ADAMS Accession No. ML19199A033). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER; therefore, no performance deficiency was identified. The inspectors did not identify a violation of NRC requirements.
- (2) LER 05000446/2018-002-01, Automatic Actuation of Auxiliary Feedwater System (ADAMS Accession No. ML19199A032). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER; therefore, no performance deficiency was identified. The inspectors did not identify a violation of NRC requirements.
INSPECTION RESULTS
Manual Reactor Trip Due to Loss of both Main Feed Pumps Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events
Green NCV 05000446/2020001-01 Open/Closed
[H.12] - Avoid Complacency 71153 A self-revealed finding and associated non-cited violation (NCV) of very low safety significance occurred when the licensee failed to implement procedures for operation of the feed and condensate system as required by Technical Specification 5.4.1a. Specifically, while adjusting flow to the auxiliary condensers for the Unit 2 main feed pumps, the licensee isolated circulating water flow to the condensers, causing a loss of both Unit 2 main feedwater pumps. Control room operators manually insert a plant trip in response to the loss of feedwater.
Description:
On January 1, 2020, the Comanche Peak on-shift operations crew decided to secure a running circulating water pump for Unit 2. Although securing the pump was not on the plan of the day schedule, the shift manager added the activity into the shift's work activities to support planned work the following week. The inspectors noted that the activity would use normal circulating water system operating Procedure SOP-310B, Circulating Water, Revision 18, and the work schedule provided enough time to prepare for and conduct the evolution. The procedure was structured to secure one circulating water pump, adjust flow as needed to the main condenser, and then to adjust flow to the two main feedwater pump auxiliary condensers. There are two steam driven main feedwater pumps.
The auxiliary condensers support operation of the two main feedwater pumps by condensing the steam used by the feedwater pump turbines. Flow was being adjusted to optimize plant thermal efficiency.
The crew successfully secured the circulating water pump and adjusted main condenser flow.
The crew then proceeded to the auxiliary condensers to adjust circulating water flow. A field operator was stationed at each of the two auxiliary condenser outlet valves and a third field operator was communicating with the main control room staff. In addition, a senior reactor operator provided local oversight of the evolution. The crew intended to adjust the throttle position of the circulating water with a final position directed by the reactor operator in the control room. The reactor operator directed the valve operators to slowly close their respective valves (simultaneously) to his mark while he monitored water box outlet temperature. The valves were initially in a throttled position at the start and they reached the fully closed position shortly after starting. Without any flow to the auxiliary condensers, both main feedwater pumps automatically tripped on low vacuum to protect the pumps. Control room staff immediately inserted a manual trip from 100 percent power. The control room operators stabilized the plant in mode 3 using Emergency Procedure E-0, Reactor Trip and Safety Injection, and normal operating procedures without further issue.
Personnel directly involved in the task failed to recognize that condenser vacuum would respond quickly to reduced cooling water flow, but there would be delays before condensate temperature would be reduced as the circulating water was adjusted due to mixing. In addition, the personnel directly involved in the task did not recognize that the auxiliary condenser outlet valves were two turns from full closed at the start of the evolution. These factors led the field operators to erroneously fully close the valves prior to control room direction to stop throttling the valves. The inspectors noted that the auxiliary condenser outlet valves had large valve position indicators to provided system configuration information to the local operators.
Comanche Peak performed a root cause evaluation to understand the event. The review identified several weaknesses in crew performance that contributed to the event. Weakness identified as the root cause were an over-reliance on process (i.e., procedures) coupled with a failure to address gaps in behaviors and standards. This resulted in a lack of critical thinking by plant staff as well as a failure to understand and address risks associated with the proposed activities. During this evolution, operators failed to recognize the potential to lose vacuum for the feed pumps due to a lack in understanding system operation and fundamentals. The crew considered the throttling of cooling water flow to be a routine activity and, therefore, the task preparations did not trigger a focused brief to discuss the evolution.
However, changing the circulating water pump configuration only occurs during winter months to allow for maintenance on the pumps. The operators assigned to the task had a lack of proficiency as none of the operators directly involved with adjusting flow on the auxiliary condensers had secured a circulating water pump before. Furthermore, the operations shift included three operators that had performed this evolution previously, but none were directly involved in adjusting flow to the auxiliary condensers. The inspectors noted that their direct involvement could have reduced the likelihood of an error during the evolution. In addition, periodic throttling of the auxiliary condenser outlet valve flow occurred with regularity; however, the adjustments were normally made in small increments with time between valve movements to allow the system to equilibrate.
The inspectors performed walkdowns of the evolution after the event, interviewed the personnel involved, reviewed plant operating procedures, and reviewed the root cause evaluation. The inspectors noted that although Comanche Peak used the correct procedure and the procedure had been used successfully previously, weaknesses in preparation for the activity and oversight led to the loss of the feed pumps. Weaknesses included a failure to recognize the risks associated with throttling auxiliary condenser circulating water flow, adjusting flow to two condensers simultaneously, giving a non-standard order (throttle slowly closed to my mark), not understanding the throttling characteristics of a butterfly valve, not establishing the initial valve positions and closely monitoring the position as it was adjusted, not monitoring the most applicable system parameters for the expected changes, and failure to recognize and compensate for a lack of proficiency of the operators in performing this evolution.
Corrective Actions: As an immediate corrective action, Comanche Peak operators tripped the Unit 2 reactor and stabilized the plant in mode 3. Personnel involved were removed from on-shift duties pending remedial training. Longer term actions included additional oversite of operations activities. Additional actions are discussed on AR 2020-00008.
Corrective Action References: CR-2020-00008
Performance Assessment:
Performance Deficiency: The failure to adequately supervise component manipulations and control system parameters within procedure limits while adjusting circulating water flow through the auxiliary condensers was a performance deficiency. Specifically, operators failed to adequately prepare for adjusting circulating water flow to the Unit 2 main feedwater pump auxiliary condenser outlet valves, which caused inappropriate valve manipulation during the evolution and created a condition that required a Unit 2 reactor trip.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the human performance attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the failure to adequately supervise component manipulations and maintain system parameters within procedural limits led to the loss of both running main feedwater pumps and a plant trip.
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. In accordance with IMC 0609, Appendix A, Exhibit 1, the inspectors determined that the finding required a detailed risk evaluation because the loss of feedwater caused operators to manually trip the reactor and the loss of main feedwater constituted a loss of mitigation equipment used to transition the plant to a stable shutdown condition.
The senior reactor analyst performed a detailed risk evaluation by treating the finding as an initiating event and using the conditional core damage probability for a loss of main feedwater as called for in Section 8.0, Initiating Event Analyses, of the Risk Assessment of Operational Events Handbook. The analyst used Comanche Peak SPAR model version 8.58, run on SAPHIRE, software version 8.2.1, for the evaluation.
The model was modified to reflect probabilistic recovery of a main feedwater pump. To accomplish this, the analyst adjusted Basic Event MFW-XHE-XL-TRIP, Operator Fails to Restart Main Feedwater Flow, used in Fault Tree MFW, Main Feedwater System, from TRUE to a SPAR-H human reliability model derived value of 4.40E-2. In this human reliability analysis, the analyst assigned high stress to both diagnosis and action and moderate complexity to both diagnosis and action for the recovery. All other performance shaping factors were set to nominal. Also, the analyst credited the use of the licensees diverse and flexible coping strategies (FLEX) equipment. Performance of the initiating event analysis with these modifications yielded an estimate of the increase in core damage frequency of 7.8E-7 per year from internal events. Loss of main feedwater events were the dominant sequences and were mitigated by the auxiliary feedwater system.
The analyst noted that this detailed risk assessment evaluates an actual event in which no external events occurred. Additionally, the period that the events impacted plant equipment was small enough that the probability of an external initiator occurring during this time would be negligible. Therefore, the analyst assumed that the risk from external events, given the subject performance deficiency, was essentially zero. This resulted a total estimate in the increase of core damage frequency of 7.8E-7 per year, making the finding of very low safety significance (Green).
The increase in large early release frequency from this finding was determined to be of very low safety significance using IMC 0609, Appendix H, Containment Integrity Significance Determination Process, because loss of main feedwater sequences screen as having low safety significance in pressurized water reactors with large dry containments.
Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. The licensee identified in their root cause analysis that operations did not recognize nor understand the risks associated with the evolution. The inspectors concluded that as a result, operators did not plan for the possibility of mistakes or implement appropriate error reduction tools.
Enforcement:
Violation: Technical Specification Section 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. NRC Regulatory Guide 1.33, Revision 2, Appendix A, Section 3, addresses Procedures for Startup, Operation, and Shutdown or Safety-Related PWR Systems and Section 3.K, addresses Feedwater System. The licensee established Procedure SOP-310B, Circulating Water, Revision 18, to address operation of the circulating water system, including adjusting flow to the auxiliary condensers which support operation of main feedwater system.
Procedure SOP-310B, Revision 18, step 5.3.7, requires operators to slowly adjust the auxiliary condenser differential pressure to between 1-and 10 feet H2O. Contrary to the above, on January 1, 2020, the licensee failed to slowly adjust the auxiliary condenser differential pressure and maintain it between 1-and 10 feet H2O when operators fully closed the valves, causing a condition (dual feedwater pump trips on low vacuum) that required a reactor trip.
Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On January 31, 2020, the inspectors presented the radiation safety exit meeting inspection results to Mr. T. McCool, Site Vice President, and other members of the licensee staff.
- On April 2, 2020, the inspectors presented the integrated inspection results to Mr. T. McCool and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Procedures
SOP-103B
Chemical and Volume Control System
Fire Plans
FPI-105B
U-2, train B Diesel generator and Equipment Elevation, 810'
Miscellaneous
Fire Hazard Analysis Report Sections 5.9.7 and 5.6
Drill 20-15-01
Fire Drill Scenario for EDG 2-02 810' Fuel Oil Transfer Pit
March 3,
20
Corrective Action
Documents
TR-YYYY-NNNN
2016-008019
Miscellaneous
Maintenance Rule Summary Report for Unit 1 and Unit 2
2/18/2020
Auxiliary Feedwater System Status
2nd Quarter
FY19
Drawings
E2-0026
6.9KV Three Line Diagram Normal Buses
Miscellaneous
STI-600.01-1
Guarded Equipment Management Posting Log
February 12,
20
Procedures
SOP-310B
Work Orders
5835726
Auxiliary Feedwater Pump Turbine 2-01Govenor Stroke
2/13/2020
Corrective Action
Documents
CR
2019-9530
2/13/2019
20-1247
February 19,
20
Drawings
M2-2760
Diesel Engine Start/Stop Logic
Operability
Evaluations
FSAR Table 8.3-1, Loading Requirements for Loss of
Coolant Accident Coincident with Loss of Offsite Power
104
CR-
20-001295
Corrective Action
Documents
CR-YYYY-NNNN
2019-009453
IR-2020-001597
Multiple Relays Out of Tolerance on Unit 2 Train B
Sequencer
Procedures
INC-7393A
CH Cal Neutron Flux Power Range ION Current Gain and
Summing Level Amplifier
MSE-S2-0673B
Unit 2 Train B Sequencer Under Voltage Relay Surveillance
Work Orders
Perform MSE-S2-0673B, TR B Sequencer UV Relay
Troubleshoot and Repair Sequence Alarm Circuit as
documented in IR-2019-009453
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Replace Cell 22 on BT1D4 at Power
Perform CCAL IAW INC-7393A
Troubleshoot test signal going to zero described in CR 2020-
001447
Miscellaneous
BEACON 3D Reactivity Projection for Unit 2 Forced Outage
Startup
01/01/2020
Procedures
ETP-106
Monthly RCCA Repositioning
OPT-106A
Control Rod Exercise
OPT-467A
Train A Safeguards Slave relay K609 Actuation Test
Revision 5
Work Orders
Solid State Protection System Slave Relay Test
March 11,
20
Perform NUC 202 AT-Power MTC Measurement
OPT-106A, Control Rod Exercise Test
Monthly RCCA Repost ETP-106
IR-2020-000542 Troubleshoot 2-01 EDG Volt Reg TRBL
Miscellaneous
ERO team Exercise
February 9,
20
Calibration
Records
3443188
X-RE-5700 ICI-4998, CCAL FB VNT EXH
06/24/2009
3648653
2-RE-6297, ICI-4961 Channel Calibration
09/30/2010
391556
1-RE-6295 ICI-4961, CCAL
03/16/2009
4373552
1-RE-6295 ICI-4961, CCAL
04/12/2016
4374577
2-RE-6297 ICI-4961, CCAL
05/10/2017
26655
X-RE-5700 ICI-4998, CCAL FB VNT EXH
01/22/2015
20934
1-RE-6256 ICI-4959 CCAL HRAM
06/09/2015
5371788
X-RE-5701 INC-4915X, CCAL AB VNT GPRM
07/18/2019
22342
1-RE-6290A INC-7079, CCAL CNTMT HRRM
05/16/2019
22458
1-RE-6290B INC-7079, CCAL CNTMT HRRM
05/02/2019
26341
1-RUK-2326A/2328A INC-4916 CCAL
07/17/2019
ASCAN
WBC System Calibration Data Package
11/20/2019
FSCAN
WBC System Calibration Data Package
09/12/2019
HP-0058
Argos/Sirius Calibration Data Sheet
11/10/2019
HP-0063
NE Technology SAM Calibration Data Sheet
10/22/2018
HP-0075
GEM-5 Calibration Data Sheet
2/04/2019
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
HP-1206
Ludlum Model 177 Frisker Calibration Data Sheet
01/27/2020
HP-2166
AMS-4 Calibration Data Sheet
10/04/2019
HP-4124
Thermo RO-20AA Calibration Data Sheet
01/29/2020
HP-5002
Low Volume Air Sampler Calibration Data Sheet
10/12/2018
HP-711812
RDS-31 Calibration Data Sheet
10/07/2019
Corrective Action
Documents
CR-YYYY-NNNN
2011-006222, 2016-001350, 2018-003694, 2018-006522,
2018-006631, 2018-007217, 2019-000184, 2019-001550,
2019-004125, 2019-004570, 2019-005318, 2019-007716,
2019-008045, 2019-008114, 2019-008129
TR-YYYY-NNNN
2018-006999, 2018-007197, 2018-007846, 2019-001511,
2019-003201, 2019-003405, 2019-003992, 2019-004146,
2019-004149, 2019-004221, 2019-005656, 2020-000063
Corrective Action
Documents
Resulting from
Inspection
CR-YYYY-NNNN
20-000750, 2020-000783, 2020-000814
Miscellaneous
1-RE-6290A
Last Detector Primary Calibration
05/15/2019
19-001 through
19-007
Calibration Well Source Charts
08/08/2019
2Qtr FY19
CPNPP System Status: Radiation Monitoring
T190990
RadCal 2026C and 1800cc, 180cc, and 6cc detectors
05/29/2019
Procedures
CLI-782
APEX Gamma Spectroscopy Counting System
ICI-4959
Channel Calibration - High Range Area Radiation Monitors
ICI-4961
Channel Calibration - Digital High Range Area Monitors
ICI-4998
Channel Calibration - Gas Process Radiation Monitor
INC-7079
Channel Calibration -
Containment High Range Radiation Monitor Channels
1-RE-6290A/B and 2-RE-6290A/B
RPI-301
Portable Survey Instruments
RPI-800
Control of Radiation Protection Equipment
RPI-802
Performance of Source Checks
RPI-862
Calibration of the Argos/Sirius Personnel Contamination
Monitor and Gem-5 Gamma Exit Monitor
STA-619
Administrative Control of Digital Radiation Monitoring System
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
STA-650
General Health Physics Plan
STA-658
Radiation Protection Equipment Calibration Program
STA-677
Preventative Maintenance Program
STA-700
Surveillance Frequency Control Program
STI-677.01
PM Change Processing
Self-Assessments EVAL-2018-006
Work Management/Radiation Protection Audit
08/02/2018
EVAL-2019-007
Chemistry Control and Chemistry Measurement & Analysis
11/21/2019
Calibration
Records
X-RE-5567A, South Plant Vent Stack Radiation Monitor
Calibration
07/30/2018
1-RE-4269, Unit 1 Station Service Water Train A to
Discharge Canal Radiation Monitor Calibration
10/24/2018
X-FT-5288, LWPS LHMT X-01/X-02 Discharge to VD System
Flow Transmitter Calibration
09/27/2018
2-RE-5100, Turbine Sump 2-04 Radiation Monitor Calibration 06/12/2019
2-RE-4269, Unit 2 Station Service Water Train A to
Discharge Canal Radiation Monitor Calibration
09/25/2019
X-RE-5253, Liquid Waste Processing Discharge Radiation
Monitor Calibration
10/28/2019
X-RE-5570B, North Plant Vent Stack WRGM Radiation
Monitor Calibration
10/01/2019
1-RE-4270, Unit 1 Station Service Water Train B to
Discharge Canal Radiation Monitor
01/14/2020
Corrective Action
Documents
CR-YYYY-NNNN
2019-008687, 2019-008794
TR-YYYY-NNNN
2017-000757, 2018-003362, 2019-001642, 2019-005866,
2019-006713, 2019-008605
Corrective Action
Documents
Resulting from
Inspection
TR-YYYY-NNNN
20-000766, 2020-000815, 2020-000817
TR-YYYY-NNNN
20-000766, 2020-000815, 2020-000817
Miscellaneous
CPSES Offsite Dose Calculation Manual, Unit 1 and Unit 2
2017 Annual Radioactive Effluent Release Report
03/12/2018
2018 Annual Radioactive Effluent Release Report
04/20/2019
G2018-034
Gaseous Discharge Permit - Unit 1 Containment Vent
2/27/2018
G2018-208
Gaseous Discharge Permit - Plant Vent Stack B
2/09/2018
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
G2018-210
Gaseous Discharge Permit - Non-Routine Gas Normal
2/10/2018
G2019-046
Gaseous Discharge Permit - Plant Vent Stack B
03/12/2019
G2019-193
Gaseous Discharge Permit - Unit 2 Containment Vent
11/24/2019
G2019-216
Gaseous Discharge Permit - Plant Vent Stack A
2/31/2019
L2018-023
Liquid Discharge Permit - Plant Effluent Tank 1
07/05/2018
L2018-040
Liquid Discharge Permit - Plant Effluent Tank 2
10/24/2018
L2018-051
Liquid Discharge Permit - Low Volume Waste Pond (LVWP)
2/01/2018
L2019-016
Liquid Discharge Permit - Plant Effluent Tank 1
2/14/2019
L2019-055
Liquid Discharge Permit - Squaw Creek Reservoir
08/01/2019
L2019-072
Liquid Discharge Permit - Plant Effluent Tank 2
2/12/2019
Procedures
CHM-170
Liquid and Gaseous Effluent Program
CHM-230
Guidelines for Sample Collection
CLI-744
Radioactive Effluent Pre-Release Permit Processing
CLI-745
Radioactive Effluent Post-Release Permit Processing and
Surveillance Tracking
STA-603
Control of Station Radioactive Effluents
STA-619
Administrative Control of the Digital Radiation Monitoring
System
STA-677
Preventive Maintenance Program
Self-Assessments EVAL-2019-007
Radioactive Waste, Effluents, Environmental, and Chemistry
Programs
11/21/2019
Work Orders
Primary Plant Ventilation Exhaust Filter Unit X-16
01/31/2018
Primary Plant Ventilation Exhaust Filter Unit X-01
10/03/2018
Primary Plant Ventilation Exhaust Filter Unit X-02
11/17/2018
Primary Plant Ventilation Exhaust Filter Unit X-02
09/18/2019
Corrective Action
Documents
CR-YYYY-NNNN
2018-001574, 2018-001611, 2018-001760, 2018-004523,
2019-002077
TR-YYYY-NNNN
2018-001867, 2018-004228, 2019-001642, 2019-007287
2019-008284, 2019-009052, 2019-009165
Corrective Action
Documents
Resulting from
Inspection
CR-YYYY-NNNN
20-000748
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Miscellaneous
2017 Annual Radiological Environmental Operating Report
04/30/2018
2018 Annual Radiological Environmental Operating Report
04/01/2019
NUPIC Audit
23724
GEL Laboratories (JQA-14-097)
05/29/2014
NUPIC Audit
24747
(NOV2019-069)
GEL Laboratories (NOD-19-018)
08/29/2019
Comanche Peak Steam Electric Station Offsite Dose
Calculation Manual Unit 1 and Unit 2
RPI-714-1-
20180715
2018 Land Use Census
07/31/2018
RPI-714-1-
20190620
2019 Land Use Census
07/25/2019
Procedures
RPI-538
Process Environmental Badges
RPI-710
Radiological Environmental Monitoring, Sampling, and
Analysis Program
RPI-713
Collection, Preparation, and Shipment of Radiological
Environmental Samples
RPI-714
Land Use Census
RPI-888
Calibration of Portable Air Sample Equipment
STA-653
Contamination Control Program
STA-654
Groundwater Protection Program
Self-Assessments EVAL-2019-007
Radioactive Waste, Effluents, Environmental, and Chemistry
Programs
11/21/2019
Work Orders
WO- 4938991, 4965490, 5052258, 5080201, 5490927,
5651858, 5654059, 5654081, 5654093, 5654106,
5654119, 5654136, 5659602, 5659645, 5667801,
5736155, 5736168, 5736197, 5736232, 5736248,
5736282, 5736299, 5741625, 5747140