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=Text=
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{{#Wiki_filter:,                                       -                                         -
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                                                                                                                                          I
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-
              gn Riog                                 UNITED STATEc                                                                     I
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                      Do.                NUCLEAP REGULATORY COMMISSION
UNITED STATEc
                      ~                                                                                                                -)
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NUCLEAP REGULATORY COMMISSION
                          n                             REGION 11
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        g'I               j                   101 MARIETTA STREET.N.W.
o.
        *     -
~
                          t                     ATLANTA, GEORGI A 30323
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                        $
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                                                                                                                                          .
REGION 11
                Report Nos.   50-413/87-42 and 50-414/87-42
g'I
                Licensee: Duke Power Company
j
                            422 South Church Street
101 MARIETTA STREET.N.W.
                            Charlotte, N.C. 28242
*
                Docket Nos.:   50-413 and 50-414                   License Nos.: NPF-35 and NPF-52
-
                Facility Name: Catcwba 1 and 2
t
                Inspection Conducted: November 26, 1987 - December 25, 1987
ATLANTA, GEORGI A 30323
                Inspector:     ~
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                                                                                                            /            7
$
                            K K 'Va'n Doorn                                                               D(ts/5igned
...
                                                /
.
                Inspector:             }})f)?//
Report Nos.
                            K 5" L&'sser'~
50-413/87-42 and 50-414/87-42
                                                          J                                                Jh W
Licensee: Duke Power Company
                                                                                                          MtVSignid
422 South Church Street
                Approved by:                     #         7                                             /' g - M
Charlotte, N.C.
                              T. A. P4ebles, Section Chief                                               Date Signed
28242
                              Pr jacts Branch 3
Docket Nos.:
                              Division of Reactor Projects
50-413 and 50-414
                                                            SUMMARY
License Nos.: NPF-35 and NPF-52
                Scope: This routine, unannounced inspection was conoucted on site inspecting-
Facility Name: Catcwba 1 and 2
                in the areas of review of plant operations; surveillv e.e observatior.;
Inspection Conducted: November 26, 1987 - December 25, 1987
                maintenance observation; review of licensee nonroutine event reports; followup
/
                of previou ly identifiad items; refueling activities (Unit 1); cold weather
7
                oreparatio.s; followup of Compliance Bulletin 87-02 and review of QA
Inspector:
                performance assessment.
K K 'Va'n Doorn
                Results:   Of the nine (9) areas inspected, one apparent violation was
/
                identif f id in one area. (Failure to Properly Classify and Report a Diesel
D(ts/5igned
~
Inspector:
}})f)?//
J
Jh W
K 5" L&'sser'~
MtVSignid
/' g - M
Approved by:
#
7
T. A. P4ebles, Section Chief
Date Signed
Pr jacts Branch 3
Division of Reactor Projects
SUMMARY
Scope: This routine, unannounced inspection was conoucted on site inspecting-
in the areas of review of plant operations; surveillv e.e observatior.;
maintenance observation; review of licensee nonroutine event reports; followup
of previou ly identifiad items; refueling activities (Unit 1); cold weather
oreparatio.s; followup of Compliance Bulletin 87-02 and review of QA
performance assessment.
Results:
Of the nine (9) areas inspected, one apparent violation was
identif f id in one area. (Failure to Properly Classify and Report a Diesel
Generator Invalid Failure
paragraph 6.c.)
.
.
.
                Generator Invalid Failure      paragraph 6.c.)
P
                                                                                      .
                                                                                                                                          P
P
P
J
J
              8801200056 8G0111
8801200056 8G0111
              PDR     ADOCK 05000413
PDR
              G                   PDR
ADOCK 05000413
  -   -   .                         ..           .                 - . - _ _ ._... . . _ . _ . . . . . . . - - - - . .   . _ _ _ . - -
G
PDR
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-
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- . -
. ... . .
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. . . . . . . - - - - . .
.
. - -


  .     -.     . _-                 . -   -               . .     .- .=       -       . - . .
.
                                                                                                                    1
-.
    . ..
. _-
                            -
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  ,                     .
-
                      .
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                                                REP 0D.T DETAILS
.
          1.   Persons Contacted
.
                'icensee Employees
.- .=
                _
-
. - . .
1
.
..
-
,
.
.
REP 0D.T DETAILS
1.
Persons Contacted
'icensee Employees
_
*H. B. Barron, Operations Superintendent
<
<
                *H. B. Barron, Operations Superintendent
W. F. Beaver; Performance Engineer
                  W. F. Beaver; Performance Engineer
W. H. Bradley, QA Surveillance
                  W. H. Bradley, QA Surveillance
S. Brown, Reactor Engineer
'
B. F. Caldwell,. Station Services Superintende t
*R. N. Casler, Operating Engineer
R. H. Charest, Station Chemistry Supervisor
*M. A. Cote, ' Licensing Specialist
*T. E. Crawford, Integrated Scheduling Superintendent
W. P. Deal, Health Physics Supervisor
C. S. Gregory, I. & E. Support Engineer
.
.,
*J. W. Hampton, Station Manager
C. L. Hartzell, Compliance Engineer
J. Knuti, Operating Engineer
F. N. Mack, Project Services Engineer
W. W. McCollough, Mechanical Maintenance Supervisce
C. E. Muse, Oper&+ing Engineer
-l
T. B. Owen, Assistant Station Manager
F. P. Schiff'ay, II, L~ censing Er.gineer
*G. T. Smith, Maintenance Superintendent
J. Stackley, I. & E. Ergineer
D. Tower, Shift Operating Engineer
*R. F. Wardell, Technical Services Superintendent
'
'
                  S. Brown, Reactor Engineer
J. W. Willis, Senior QA Engineer, Operations
                  B. F. Caldwell,. Station Services Superintende t
Other licensee employees contacted included technicians, operators,
                *R.      N. Casler, Operating Engineer
)
                  R. H. Charest, Station Chemistry Supervisor
                *M. A. Cote, ' Licensing Specialist
                *T. E. Crawford, Integrated Scheduling Superintendent
                  W. P. Deal, Health Physics Supervisor
                  C. S. Gregory, I. & E. Support Engineer                                                      .,
                                                                                                                  .
                *J. W. Hampton, Station Manager
                  C. L. Hartzell, Compliance Engineer
                  J. Knuti, Operating Engineer
                    F. N. Mack, Project Services Engineer
                  W. W. McCollough, Mechanical Maintenance Supervisce
                  C. E. Muse, Oper&+ing Engineer                                                              -l
                  T. B. Owen, Assistant Station Manager
                    F. P. Schiff'ay, II, L~ censing Er.gineer
                *G. T. Smith, Maintenance Superintendent
                  J. Stackley, I. & E. Ergineer
                  D. Tower, Shift Operating Engineer
                *R.      F. Wardell, Technical Services Superintendent                                            '
                  J. W. Willis, Senior QA Engineer, Operations
"
"
                Other licensee employees contacted included technicians, operators,                                )
mechanics, security force members, and office personnel.
                mechanics, security force members, and office personnel.                                           ;
:)
                                                                                                                :)
2.
          2.   Exit laterview                                                                                 ]H
Exit laterview
                Tra inspection scope and findings were summarized on December 23, 1981,                             I
]
                with those persons indicated in paragraph 1 above.           The inspector                         l
H
                described the areas inspected and discussed in detail the inspection                               !
Tra inspection scope and findings were summarized on December 23, 1981,
with those persons indicated in paragraph 1 above.
The inspector
described the areas inspected and discussed in detail the inspection
findings.
Dissenting comments were not received from the licensee.
'
'
                findings.      Dissenting comments were not received from the licensee.
'
                                                                                                                    '
Proprietary information is net contained in this report.
                Proprietary information is net contained in this report.       The folicwing
The folicwing
                new items were identified:                                                                         1
new items were identified:
                                                                                                                    l
1
.                Unresolved Item 413/87-42-01: C'osed KC Supply Valve to RHR V         ichanger                     i
Unresolved Item 413/87-42-01: C'osed KC Supply Valve to RHR V
                in Service.                                                                                         l
ichanger
                Violation 413/87-42-02: Failure to Properly Classify and Repo-         . Diesel.                   I
.
                Generator Invalid Failure.                                                                         '
in Service.
                                                                                                                    i
Violation 413/87-42-02: Failure to Properly Classify and Repo-
              -           -   -             .     .   , , - -     -   ,-       .-   ..a.-         .. - . - ,
Diesel.
.
Generator Invalid Failure.
'
i
-
-
-
.
.
, , - -
-
,-
.-
..a.-
..
- . - ,


              . -       . .                                 .     .       .-     -                 .-           .
. -
    .             .
. .
                                                        -
.
                                            .
.
                                -
.-
                                          .
-
                                                                                                    '2
.-
                                                                                                                                                  .
.
                                        Unresolved. Item 413/87-42-03: . Inadequate Test Procedure for Blackout-
.
                                        Testing During Solid Plant Operations.
.
                            3.         Licensee Action on Previous Enforcement _ Matters (92702)
-
.
-
.
'2
.
Unresolved. Item 413/87-42-03: . Inadequate Test Procedure for Blackout-
Testing During Solid Plant Operations.
3.
Licensee Action on Previous Enforcement _ Matters (92702)
a.
(CLOSED)
Unresolved Item 413,414/87-05-01: Management Review ano
,
,
,
  ,
Corrective Action of Excessive Problems Occurring on a Specific
                                        a.        (CLOSED)        Unresolved Item 413,414/87-05-01: Management Review ano
'
'
                                                  Corrective Action of Excessive Problems Occurring on a Specific
Assigned Shift. The licensee has counseled appropriate personnel and
                                                Assigned Shift. The licensee has counseled appropriate personnel and
the Snift Supervisor has implemented improvements in communications
                                                  the Snift Supervisor has implemented improvements in communications
on shift. The inspe tors have regu'larly observed this shif t crew and
                                                  on shift. The inspe tors have regu'larly observed this shif t crew and
have not observed any additional significant . problems. Therefore,
                                                  have not observed any additional significant . problems. Therefore,
this item is closed.
                                                  this item is closed.
b.
                                        b.       (CLOSED) Unresolved Itna 413/87-36-04: Icability of PORV's to Fail
(CLOSED) Unresolved Itna 413/87-36-04: Icability of PORV's to Fail
                                                  Scfe Clocod. NRC:RII personnel reviewed the licensee's "operability
Scfe Clocod.
                                                  detarmination" of, the Pressurizer PORV's and found it to be
NRC:RII personnel reviewed the licensee's "operability
                                                  accep;Tble.           The licensee additior,sily was able to -correct problems
detarmination" of, the Pressurizer PORV's and found it to be
                                                  with the valves and meet required stroke times under "fail safe"
accep;Tble.
                                                  conditions.           Based on thin the item is closed.
The licensee additior,sily was able to -correct problems
                                                  No violations or dev. .t.ons .-ere ideatified.
with the valves and meet required stroke times under "fail safe"
                            4.         Unresolved items *
conditions.
                                        hew unresolved items are' identified in paragraphs 5.b. and 6.d.
Based on thin the item is closed.
                            5.         Plant Operations Review (71707 c.nd 71710)
No violations or dev. .t.ons .-ere ideatified.
                                        a.         The inspectors reviewed plant cperations throughout the reportin'g                             >
4.
                                                  period to verify ccnformance with regulatory *equirements, ' Technical
Unresolved items *
                                                  Specifications (TS), and administrative controls. Control recm logs,
hew unresolved items are' identified in paragraphs 5.b. and 6.d.
5.
Plant Operations Review (71707 c.nd 71710)
a.
The inspectors reviewed plant cperations throughout the reportin'g
>
period to verify ccnformance with regulatory *equirements, ' Technical
Specifications (TS), and administrative controls. Control recm logs,
danger tag logs, Technical Specification Action Item Log, and the
,
removal and restoration log were routinely reviewed. Shift turnovers
were observed to verify that they were conducted in accordance with
approved procedures.
,
,
                                                  danger tag logs, Technical Specification Action Item Log, and the
. i
                                                  removal and restoration log were routinely reviewed. Shift turnovers
The inspectors. verified by observation and interviews,-that measures
                                                  were observed to verify that they were conducted in accordance with
                                                  approved procedures.                                                                           ,
                                                                                                                                                .i
-
-
                                                  The inspectors. verified by observation and interviews,-that measures
taken to a ssure physical protection of the facility met current
                                                  taken to a ssure physical protection of the facility met current                             .;
. ;
,                                                  requiremen             Areas inspected included the security organization,                     !
requiremen
.                                                  the estahl ,,iment and maintenances of gates, r.;c-s, and isolation                             '
Areas inspected included the security organization,
,
the estahl ,,iment and maintenances of gates,
r.;c-s, and isolation
'
.
zones in the proper condition, that access cc xc1 and badging were
-
-
proper and procedures followed.
j
"
"
                                                  zones in the proper condition, that access cc xc1 and badging were
* An Unresolved Item is a matter which more information is required to dete?_
                                                  proper and procedures followed.                                                                j
,
                                                                                                                                                  !
mined whether it is acceptable or may involve a violation or deviation.
                            * An Unresolved Item is a matter which more information is required to dete?_                                         ,
                            mined whether it is acceptable or may involve a violation or deviation.                                               I
,
,
9
9
                                                                                                                              ?
?
      , , - -       , ,,         ..,--       - - - - ,   ,,   --,,,,nw     r- c   , , , , , , . ,   , , . ,   ,. - - , ,   ,,, , , - - . .
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  ..y .
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                                .. ..                            ._ _        _.      .  -    _                        _        _ __
      .
                            -
.
.
                                                                3-
..
                        In addition to the areas discussed above, .tl , areas toured were
..
                        observed for fire prevention and protection activities.                       These
._ _
                        included such things-as combustible. material control, fire protection
_.
                        systems ~ and materials,; and-. fire protection associated with                                               ,
.
                        maintenance   activities.             The       inspectors -reviewed     Problem
-
                        Investigation Reports (PIRs) to . determine if - the licensee was
_
                        appropriately documenting problems and implementing appropriate
_
                        corrective actions.
_ __
                b.     The inspectors conducted t. detailed walkdown.of tFe Unit 1 component
.
                        cooling system and the Unit 2 Diesel Generator. A and B train
-
                        electrical switchgear.             The following discreparcies were noted and                                 !
.
                        forwarded to the licensee for followup correction: The - terminal box
3-
                        on Limitorque operator for 1KC-2B was missing a drain plug and
In addition to the areas discussed above, .tl
                        tarminal box covers screws were either loose or missing from 1KC-2B
, areas toured were
                        and 1KC-1A.
observed for fire prevention and protection activities.
                        It was also noted that IKC-81B, KC Supply Valve to IB Residual Heat
These
                        Removal (ND) Heat Exchanger, was shut although B train ND was in
included such things-as combustible. material control, fire protection
                        service per T.S. 3.4.1.4.1. for decay heat removal. 0P/1/A/6200/04,
systems ~ and materials,; and-. fire protection associated with
                        Residual Heat Removal System, requires this valve to be open.                       The
,
                        inspectors were told that it was closed because the NU throttle
maintenance
                        valve, was not functioning properly, allowing ~ excessive ND to flow
activities.
                        through the heat exchanger, and 1KC-818. leaked by enough wh'~ fully
The
                        closed suen that it could be closed to reduce cooling f'                           The
inspectors -reviewed
                        inspectors noted TC flow through the heat exchanger to be approx-
Problem
                        imately 1300 gpm with 1KC-510 closed. The inspectors were also. told
Investigation Reports (PIRs) to . determine if - the licensee was
                        that there had not been a work request initiated on 1KC-81B,-nor was
appropriately documenting problems and implementing appropriate
                        there a Restoration and Removal record or an op.en item associated
corrective actions.
                        with the valve. The liceasee was asked.to review its procedures for
b.
                        edequacy of requirements to ensure proper authorization is obtained
The inspectors conducted t. detailed walkdown.of tFe Unit 1 component
                        and reccrds are maintained when a valve is placed in a position other
cooling system and the Unit 2 Diesel Generator. A and B train
                        than that stated by the procedure. This is identified as Unresolved
electrical switchgear.
                        item 413/87-42-01 Closod KC Supply Valve to RHR Heat Exchanger in
The following discreparcies were noted and
                        Service, pending NRC and licensee review of prc:edural adequacy to
!
                        maintain control over valve positions.
forwarded to the licensee for followup correction: The - terminal box
                c.     Unit 2 Summary
on Limitorque operator for 1KC-2B was missing a drain plug and
7                       The Unit started the reporting period at 75% power,. coasting down in-
tarminal box covers screws were either loose or missing from 1KC-2B
                        prepa*atior. for first refueling outage which was scheduled to
and 1KC-1A.
                        commence December 18. Due to delays in the Unit refueling, it was
It was also noted that IKC-81B, KC Supply Valve to IB Residual Heat
                        determined to extend Unit 2 operation for 5 extra days and power was
Removal (ND) Heat Exchanger, was shut although B train ND was in
                        reduced to 65%.             Unit 2 shutdown to commence its first refueling
service per T.S. 3.4.1.4.1. for decay heat removal. 0P/1/A/6200/04,
                        outage on December 23.
Residual Heat Removal System, requires this valve to be open.
The
inspectors were told that it was closed because the NU throttle
valve, was not functioning properly, allowing ~ excessive ND to flow
through the heat exchanger, and 1KC-818. leaked by enough wh'~ fully
closed suen that it could be closed to reduce cooling f'
The
inspectors noted TC flow through the heat exchanger to be approx-
imately 1300 gpm with 1KC-510 closed. The inspectors were also. told
that there had not been a work request initiated on 1KC-81B,-nor was
there a Restoration and Removal record or an op.en item associated
with the valve. The liceasee was asked.to review its procedures for
edequacy of requirements to ensure proper authorization is obtained
and reccrds are maintained when a valve is placed in a position other
than that stated by the procedure. This is identified as Unresolved
item 413/87-42-01 Closod KC Supply Valve to RHR Heat Exchanger in
Service, pending NRC and licensee review of prc:edural adequacy to
maintain control over valve positions.
c.
Unit 2 Summary
7
The Unit started the reporting period at 75% power,. coasting down in-
prepa*atior. for first refueling outage which was scheduled to
commence December 18.
Due to delays in the Unit refueling, it was
determined to extend Unit 2 operation for 5 extra days and power was
reduced to 65%.
Unit 2 shutdown to commence its first refueling
outage on December 23.
No violations or deviattor.s were identified.
''
''
                        No violations or deviattor.s were identified.
'l
'l
                                                                                                          Y
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r
                                                                                                ..     ~-,     m,...- . . - - , ~ .
. , ~ , . _
.
.,,_. . - . . , -
_
,
,,
,
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..
~-,
m,...-
. . - - , ~ .


  .   -                       -           .     -     _.         -       _.               . .
.
    .
-
                    .
-
                                                  4
.
        6. Surveillance Observation (61726)
-
            a. During the inspection period, the inspector verified plant
_.
                operations were in compliance with various TS requirements. Typical
-
                of these requirements were confirmation of compliance with the TS
_.
                for reactor coolant chemistry, refueling water _ tank, emergency - power-
.
                systems, safety injection, emergency safeguards systems,, control room-
.
                ventilation, and direct current electrical power sources.           The
.
                inspector verified that surveillance testing lwas performed in
.
                accordance with'the approved written procedures, test instrumentation
4
                was calibrated, limiting conditions for operation were met, appro-
6.
                priate removal and restoration of the affected equipment- was
Surveillance Observation (61726)
                accomplished, test results met requirements and were reviewed by
a.
                personnel other than the individual directing the test, and that any
During the inspection period, the inspector verified plant
                deficiencies identified during the testing were properly reviewed and
operations were in compliance with various TS requirements. Typical
                resolved by appropriate management personnel.
of these requirements were confirmation of compliance with the TS
            b.   The following surveillance activity was witnessed:
for reactor coolant chemistry, refueling water _ tank, emergency - power-
                PT/1/A/4200/09         Train B Safety Injection, Phase'A, Phase B, and
systems, safety injection, emergency safeguards systems,, control room-
                                        Blackout Testing.
ventilation, and direct current electrical power sources.
            c.   On November 13, 1987 the 1A Diesel Generator tripped after start
The
,                number 548 due to the P-3 shuttle valve failing to seat properly.
inspector verified that surveillance testing lwas performed in
l
accordance with'the approved written procedures, test instrumentation
                This valve vents control air pressure on emergency trip signals to               -
was calibrated, limiting conditions for operation were met, appro-
                shutdown the engine.     Operations Management Procedure- (OMP) 2-28.
priate removal and restoration of the affected equipment- was
                Diesel Generator Logbook, requires tuat each diesel generator start
accomplished, test results met requirements and were reviewed by
                attempt be classified as a Valid Success / Failure or Invalid Test /
personnel other than the individual directing the test, and that any
                Failure. The licensee failed to properly classify the trip as an
deficiencies identified during the testing were properly reviewed and
                                                                          _
resolved by appropriate management personnel.
                invalid failure until prompted by the' NRC resident inspectors.
b.
                Following discussions with the licensee personnel, an intrastation         ,
The following surveillance activity was witnessed:
                  letter dated December 9,1987 from R.N. Casler to Lee Hartzell was
PT/1/A/4200/09
                  issued which reclassified the trip from an invalid test to an invalid
Train B Safety Injection, Phase'A, Phase B, and
                failure.     Consequently the itcensee failed to report the diesel
Blackout Testing.
                generator failure to the NRC within 30 days per T.S. 4.8.1.1.3.       This
c.
                constitutes a violation of T.S. 4.8.1.1. 3 and 6.8.1.         Violation
On November 13, 1987 the 1A Diesel Generator tripped after start
                413/87-42-02: Failure to Properly Classify and Report a Diesel
number 548 due to the P-3 shuttle valve failing to seat properly.
                Generator Invalid Failure.
,
                The resident inspectors reviewed the Diesel Generator Logbooks as
l
                  part of this investigation and noted numerous errors indicating that
This valve vents control air pressure on emergency trip signals to
-
shutdown the engine.
Operations Management Procedure- (OMP) 2-28.
Diesel Generator Logbook, requires tuat each diesel generator start
attempt be classified as a Valid Success / Failure or Invalid Test /
Failure.
The licensee failed to properly classify the trip as an
_
invalid failure until prompted by the' NRC resident inspectors.
Following discussions with the licensee personnel, an intrastation
,
letter dated December 9,1987 from R.N. Casler to Lee Hartzell was
issued which reclassified the trip from an invalid test to an invalid
failure.
Consequently the itcensee failed to report the diesel
generator failure to the NRC within 30 days per T.S. 4.8.1.1.3.
This
constitutes a violation of T.S.
4.8.1.1. 3 and 6.8.1.
Violation
413/87-42-02: Failure to Properly Classify and Report a Diesel
Generator Invalid Failure.
The resident inspectors reviewed the Diesel Generator Logbooks as
part of this investigation and noted numerous errors indicating that
increased attention is necessary in tracking and evaluating diesel
,
,
                  increased attention is necessary in tracking and evaluating diesel
starts. The Test Failure / Invalid Test Description Sheet for the IB
'
'
                  starts. The Test Failure / Invalid Test Description Sheet for the IB
diesel generator valid failure on start number 719 had not been
                diesel generator valid failure on start number 719 had not been
initiated. As of December 18, Description Sheets for starts 718-751
                  initiated. As of December 18, Description Sheets for starts 718-751               j
j
                on the 18 diesci generator, done between December 1-5, had not been
on the 18 diesci generator, done between December 1-5, had not been
                  reviewed by the Unit Coordinator or his designee and approximately 4             i
reviewed by the Unit Coordinator or his designee and approximately 4
                  of these starts had not been reviewed by the Shift or Unit
i
                                                                                                    l
of these starts had not been reviewed by the Shift or Unit
                                                                                                  1
1
                                                                                                    i
i
                                                                                      5-
5-


.
.
            .
.
                                          5
5
          Supervisor.   OMP 2-29 requires these reviews to be completed within
Supervisor.
          seven days.   Finally the index of the logbook had two separate starts
OMP 2-29 requires these reviews to be completed within
          on different dates identified as start number 718. The licensee
seven days.
          acknowledged weaknesses in this area and agreed that increased
Finally the index of the logbook had two separate starts
          supervisory attention is required.
on different dates identified as start number 718.
          The inspectors also held discussions with the licensee to clarify the
The licensee
          reportability and classification requirements of Regulatory Guide
acknowledged weaknesses in this area and agreed that increased
          1.108 Rev.1, Periodic Testing of Diesel Generator Units as Onsite
supervisory attention is required.
          Electric Power Systems at Nuclear Plants.       The licensee agreed to
The inspectors also held discussions with the licensee to clarify the
          revise OMP 2-28 to ensure specifically that diesel
reportability and classification requirements of Regulatory Guide
          generator valid and invalid failures were properly classified and
1.108 Rev.1, Periodic Testing of Diesel Generator Units as Onsite
          reported.
Electric Power Systems at Nuclear Plants.
    d.   On December 3,   1987   "B" train blackout ESF testing was being
The licensee agreed to
          conducted on Unit I while the plant was solid. Reactor Coolant (NC)
revise OMP 2-28 to ensure specifically that diesel
          System pressure was being maintained at approximately 325 psig. Both
generator valid and invalid failures were properly classified and
          trains of Component Cooling (KC) were supplying the         "A" train
reported.
          Residual Heat Removal (ND) heat exchanger. Upon initiating a
d.
          blackout signal on "B" train 4160 KV bus, B train KC pumps were
On December 3,
          de-energized until the IB diesel generator started and sequenced on
1987
          the pumps. The partial loss of KC caused the NC system to heat up
"B"
          slightly, however since the plant was solid a large pressure increase
train blackout ESF testing was being
          occurred and resulted in the pressurizer power operated relief valve
conducted on Unit I while the plant was solid. Reactor Coolant (NC)
          (PORV) setting of 400 psig being exceeded. One PORV opened to
System pressure was being maintained at approximately 325 psig. Both
          relieve the pressure.     The testing was initially intended to be
trains of Component Cooling (KC) were supplying the
          performed when the plant was not solid however problems with
"A"
          equipment forced a delay. Apparently the consequences of losing one
train
          train of KC while solid were inadequately evaluated prior to approvhl
Residual Heat Removal (ND) heat exchanger.
          of the test.   This is identified as Unresolved Item 413/87-42-03:
Upon initiating a
          Inadequate Test Procedure for Blackout Testing During Solid Plant
blackout signal on
          Operations, pending further review by the inspectors.
"B"
          Cne violation was identified as described in paragraph 6.c. above.
train 4160 KV bus, B train KC pumps were
  7. Maintenance Observations (62703)
de-energized until the IB diesel generator started and sequenced on
    a.   Station maintenance activities of selected systems and components
the pumps. The partial loss of KC caused the NC system to heat up
          were observed / reviewed to ascertain that they were conducted in
slightly, however since the plant was solid a large pressure increase
          accordance with requirements.       The inspector verified licensee
occurred and resulted in the pressurizer power operated relief valve
          conformance to the requirements in the following areas of inspection:
(PORV) setting of 400 psig being exceeded.
          the activities were accomplished using approved procedures, and
One PORV opened to
          functional testing and/or calibrations were performed prior to
relieve the pressure.
          returning components or systems to service; quality control records
The testing was initially intended to be
          were maintained; activities performed were accomplished by qualified
performed when the plant was not solid however problems with
          personnel; and materials used were properly certified. Work requests
equipment forced a delay. Apparently the consequences of losing one
          were reviewed to determine status of outstanding jobs and to assure
train of KC while solid were inadequately evaluated prior to approvhl
          that priority is assioned to safety-related equipment maintenance
of the test.
          which may effect systam performance.
This is identified as Unresolved Item 413/87-42-03:
Inadequate Test Procedure for Blackout Testing During Solid Plant
Operations, pending further review by the inspectors.
Cne violation was identified as described in paragraph 6.c. above.
7.
Maintenance Observations (62703)
a.
Station maintenance activities of selected systems and components
were observed / reviewed to ascertain that they were conducted in
accordance with requirements.
The inspector verified licensee
conformance to the requirements in the following areas of inspection:
the activities were accomplished using approved procedures, and
functional testing and/or calibrations were performed prior to
returning components or systems to service; quality control records
were maintained; activities performed were accomplished by qualified
personnel; and materials used were properly certified. Work requests
were reviewed to determine status of outstanding jobs and to assure
that priority is assioned to safety-related equipment maintenance
which may effect systam performance.


      . _                 _                   _                                                         _. .
. _
  . .
_
                                                                                                                        l
_
                    :
_.
                                                                                                                        i
.
                                                              6
.
                                                                                                                        1
.
                                                                                                                        1
:
              b.           The inspector witnessed portions of. the 'following maintenance                               !
6
                          activity in progress:
1
                          PT/1/A/4200/23A         -Post Maintenance Stroke Timing of.PORV 1NC-34A_
b.
                          No violations or deviations were identified.
The inspector witnessed portions of. the 'following maintenance
          8. Review of Licensee Nonroutine Event Reports ~(92700)
activity in progress:
              a.           The below listed Licensee Event Reports (LER) were' reviewed to
PT/1/A/4200/23A
                          determine if the information provided met NRC requirements. .The
-Post Maintenance Stroke Timing of.PORV 1NC-34A_
                          determination included: adequacy of description, verification of
No violations or deviations were identified.
                          compliance with Technical Specifications and regulatory requirements,
8.
                          corrective action taken, existence of potential generic problems,
Review of Licensee Nonroutine Event Reports ~(92700)
                          reporting requirements satisfied, and the relative- safety
a.
                          significance of each -event.           Additional implant reviews and
The below listed Licensee Event Reports (LER) were' reviewed to
                          discussion with plant personnel, as appropriate, were conducted for
determine if the information provided met NRC requirements. .The
                          those reports indicated by an (*).         The following LERs are closed:               ,
determination included: adequacy of description, verification of
                                                                                                                      '
compliance with Technical Specifications and regulatory requirements,
                          *413/85-53 Rv.1         Diesel Generator IA Battery Charger Inoperable
corrective action taken, existence of potential generic problems,
                                                    Due to Blown Fuses
reporting
                          *413/86-58 Rv.1         Reactor Trip and Feedwater Isolation Due to an
requirements
                                                    Unexpected Response from RTD Simulator
satisfied,
                              413/87-38             Missed Hourly Fire Watches Result in TS
and
                                                    Violation Due to a Personnel Error
the
                          *413/87-40               Turbine Driven Auxiliary Feedwater Pump                           !
relative- safety
                                                    Auto-Start Signal / Steam Generator Blowdown
significance of each -event.
                                                    Containment Isolation Valves Actuation Due to
Additional
                                                    Procedural Deficiency
implant reviews and
                          *414/87-07 Rv.1         Reactor Trip Due to a Management Deficiency and
discussion with plant personnel, as appropriate, were conducted for
                                                    Equipment Failures
those reports indicated by an (*).
              b.           On November 5,       1987 with Unit 2 in Mode 4, a Main Feedwater (CF)
The following LERs are closed:
                          Isolation and an Auxiliary Feedwater (CA) Auto Start occurred when
,
                          IAE technicians shut the root valve for Steam Generator 2C Narrow
'
                          Range level Channel IV instead of Channel II. When the line was
*413/85-53 Rv.1
                          vented the 2/4 logic for Hi Hi Steam Generator level was made up.
Diesel Generator IA Battery Charger Inoperable
                          This incident is described in LER 414/87-30. The root cause of the
Due to Blown Fuses
                          event is an apparent personnel error in that the technicians did not
*413/86-58 Rv.1
                          properly identify the correct component.           The technicians however;
Reactor Trip and Feedwater Isolation Due to an
                          were severely hampered by inadequate root valve labeling and                               1
Unexpected Response from RTD Simulator
                            instrument detail drawings that are vague, cluttered and difficult to_                   '
413/87-38
                          comprehend. A Station Problem Report has been initiated to review                         a
Missed Hourly Fire Watches Result in TS
                            steam generator level channel drawings and the licensee intends to
Violation Due to a Personnel Error
                                                                                                                      '
!
i                         effectively label steam generator and pressurizer instrument valves.
*413/87-40
                                                                                  ,
Turbine Driven Auxiliary Feedwater Pump
                                                                                                                      f
Auto-Start
;                                                                                                       -
Signal / Steam
            .   _ . _ - -         .
Generator
                                        .. .._                . -. .   _   . _          .-_ _ _ ..       ._._
Blowdown
Containment Isolation Valves Actuation Due to
Procedural Deficiency
*414/87-07 Rv.1
Reactor Trip Due to a Management Deficiency and
Equipment Failures
b.
On November 5,
1987 with Unit 2 in Mode 4, a Main Feedwater (CF)
Isolation and an Auxiliary Feedwater (CA) Auto Start occurred when
IAE technicians shut the root valve for Steam Generator 2C Narrow
Range level Channel IV instead of Channel II.
When the line was
vented the 2/4 logic for Hi Hi Steam Generator level was made up.
This incident is described in LER 414/87-30. The root cause of the
event is an apparent personnel error in that the technicians did not
properly identify the correct component.
The technicians however;
were severely hampered by inadequate root valve labeling and
1
instrument detail drawings that are vague, cluttered and difficult to_
'
comprehend. A Station Problem Report has been initiated to review
a
steam generator level channel drawings and the licensee intends to
'
i
effectively label steam generator and pressurizer instrument valves.
,
f
;
-
.
.
- -
.
.. ..
.
-. .
_
.
.-
..
._._


          _ .   _                 .               .     .                       _ _.   - _ _ _
_ .
                                                                                                      _ _ . _
_
    .   .
.
                          '
.
      '
.
                    .'
_ _.
                                                      7
- _ _ _
  .                    These same' problems with instrument' labeling and detail drawings
_ _ . _
                      possibly go beyond the steam generators and pressurizer. The Duke
.
                      Power Labeling Committee has been established to label plant-
.
                      components and. valves. This LER remains open pending further review
'
                      by the inspectors.into the personnel error and the labeling program.
'
                c.   LER 413/87-39 discussed ' corrective action for a spurious CA
.'
                      auto-start due to the ' simultaneous implementation of 2 Nuclear
7
                      Station' Modifications (NSM).   The corrective action includes- adding
These same' problems with instrument' labeling and detail drawings
                      information to test procedures which state that CA auto-start will
.
                      occur if an auto-start signal is received due to other maintenance
possibly go beyond the steam generators and pressurizer.
                      activities in progress while Solid State Protection System (SSPS) is
The Duke
                      in test. The LER further states that these procedure changes will
Power Labeling Committee has been established to label plant-
                      make CA auto-starts, under these conditions, not reportable.       The
components and. valves. This LER remains open pending further review
                      inspectors informed the licensee that 10CFR 50.73 and NUREG 1022
by the inspectors.into the personnel error and the labeling program.
                      clearly does not exempt these spurious ESFs from being reportable
c.
                      unless the licensee can show that the actuation was part of a
LER 413/87-39 discussed ' corrective action for a spurious CA
                      preplanned sequence during testing or operation.     The licensee was
auto-start due to the ' simultaneous implementation of 2 Nuclear
                      asked to ensure this policy'is clearly understood by its personnel.
Station' Modifications (NSM).
                      The licensee was also informed that since the wording in the LER
The corrective action includes- adding
                      might imply otherwise, it would be appropriate to submit a supple-
information to test procedures which state that CA auto-start will
                      mented LER elaborating on the corrective actions.
occur if an auto-start signal is received due to other maintenance
                      No violations or deviations were identified.
activities in progress while Solid State Protection System (SSPS) is
              9. Refueling Activities and Startup After Refueling (Unit 1) (60710 & 71711)
in test. The LER further states that these procedure changes will
                a.   The inspectors verified that T.S. applicable to Modes 4, 5, and 6
make CA auto-starts, under these conditions, not reportable.
                      were met, reactor coolant level control practices were followed,
The
                      containment cleanliness inspections and cleanup was adequate and
inspectors informed the licensee that 10CFR 50.73 and NUREG 1022
                      procedures were in use ensure systems disturbed or tested during the
clearly does not exempt these spurious ESFs from being reportable
unless the licensee can show that the actuation was part of a
preplanned sequence during testing or operation.
The licensee was
asked to ensure this policy'is clearly understood by its personnel.
The licensee was also informed that since the wording in the LER
might imply otherwise, it would be appropriate to submit a supple-
mented LER elaborating on the corrective actions.
No violations or deviations were identified.
9.
Refueling Activities and Startup After Refueling (Unit 1) (60710 & 71711)
a.
The inspectors verified that T.S. applicable to Modes 4, 5, and 6
were met, reactor coolant level control practices were followed,
containment cleanliness inspections and cleanup was adequate and
procedures were in use ensure systems disturbed or tested during the
outage were returned to operable status.
-
-
                      outage were returned to operable status.
b.
                b.    Unit 2 Summary
Unit 2 Summary
                                                                                                                l
The
                      The  unit completed containment     Intergrated Leak Rate Test                         i
unit completed containment
                      successfully on November 25. The test was witnessed by the resident
Intergrated
                      and regional inspectors.   The unit also entered Mode 5 on November                     1
Leak
                      25. On December 10 a borated water leak of 1-2 gpm was discovered on
Rate
                      a Control Rod Drive Mechanism (CRDM) Vent plug. The leak had been in
Test
                      existence for 24-36 hours and spilled borated water on the vessel
i
                      head and wetted CRDM cabling and rod position indication cabling. An
successfully on November 25. The test was witnessed by the resident
                      extensive cleanup effort was required which included removal of boron
and regional inspectors.
                      crystals and drying out and testing electrical cabling. To perform
The unit also entered Mode 5 on November
                      this the outage had to be extended an additional two weeks.
1
                      Concurrently with discovering the vent plug leak the licensee
25. On December 10 a borated water leak of 1-2 gpm was discovered on
                      discovered evidence to indicate a small primary to secondary leak in
a Control Rod Drive Mechanism (CRDM) Vent plug. The leak had been in
                      the 1A Steam Generator. Efforts to locate the leaking tube included
existence for 24-36 hours and spilled borated water on the vessel
                                                                                                                i
head and wetted CRDM cabling and rod position indication cabling. An
                                                                                                                !
extensive cleanup effort was required which included removal of boron
                                                                                                                !
crystals and drying out and testing electrical cabling. To perform
                                                                                                                l
this the outage had to be extended an additional two weeks.
                                                                                                                l
Concurrently with discovering the vent plug leak the licensee
                                                                                                  ..-         -l
discovered evidence to indicate a small primary to secondary leak in
the 1A Steam Generator. Efforts to locate the leaking tube included
i
..-
- l


                                                                                      . - - . _ -
. - -
. .- .. ,
. _ -
                      .
. .-
                .
..
                                                  8
,
                  pressurizing .the tscondary. side to 800 psig and inspecting for' tube
.
                  in leakage, however were unsuccessful. The licensee estimated the               ,
.
                  leak rate to be 17 gallons per day from detected activity levels in
8
                  the secondary. The resident inspectors will' closely monitor licensee
pressurizing .the tscondary. side to 800 psig and inspecting for' tube
                  activities to better quantify the leak during startup. The unit
in leakage, however were unsuccessful. The licensee estimated the
                  entered Mode 4 on' December 22 and Mode 3 on December 23.
,
                  No violations or deviations were identified.
leak rate to be 17 gallons per day from detected activity levels in
        10. Previously Identified Inspector Findings (92701)
the secondary. The resident inspectors will' closely monitor licensee
            (CLOSED)   Inspector Followup Item 87-07-01: Failure to Demonstrate
activities to better quantify the leak during startup.
            Adequate Access Control Measures, for the OSC as Stated in Exercise
The unit
            Objective B.1.K.     The . licensee has determined that the objective was
entered Mode 4 on' December 22 and Mode 3 on December 23.
            inappropriate for the exercise since the.0SC is inside the protected area.
No violations or deviations were identified.
            In addition the OSC Coordinator has been charged with controlling any
10.
            access problems and has the authority to have personnel removed. Licensee
Previously Identified Inspector Findings (92701)
            actions are acceptable.
(CLOSED)
            No violations or deviations were identified.
Inspector Followup Item 87-07-01: Failure to Demonstrate
        11. Cold Weather Preparations (71714)
Adequate Access Control Measures, for the OSC as Stated in Exercise
            The inspectors verified that the licensee was inspecting / repairing cold
Objective B.1.K.
            weather protection devices in preparation for the winter season.       Work
The . licensee has determined that the objective was
            Request 3057 SWR for inspection of thermostats, heaters and. instrumen-
inappropriate for the exercise since the.0SC is inside the protected area.
            tation boxes had been implemented. Additional Work Requests 8601 IAE and
In addition the OSC Coordinator has been charged with controlling any
            8606 IAE were issued to complete required repairs. The inspector reviewed
access problems and has the authority to have personnel removed. Licensee
            documentation on the Work Requests which showed that all repairs had been
actions are acceptable.
            made except for- replacement of some rusted screws on one heater box. In
No violations or deviations were identified.
            addition, the inspector observed the Refueling Water Storage Tank level
11. Cold Weather Preparations (71714)
              instrument loops on both units. Minor insulation damage was noted on Loop
The inspectors verified that the licensee was inspecting / repairing cold
            No. 2FWLT 5010. The licensee was informed of this damage.
weather protection devices in preparation for the winter season.
            No violations or deviations were identified.
Work
        12.   Followup of Compliance Bulletin 87-02, Fastener Testing to Determine
Request 3057 SWR for inspection of thermostats, heaters and. instrumen-
            Conformance with Applicable Material Specifications (25026)
tation boxes had been implemented. Additional Work Requests 8601 IAE and
            The inspectors reviewed the licensee selection process for fasteners to be
8606 IAE were issued to complete required repairs. The inspector reviewed
                                                                                                  j
documentation on the Work Requests which showed that all repairs had been
                                                                                                  )
made except for- replacement of some rusted screws on one heater box. In
              tested as required by the Bulletin.     The inspectors also observed the             !
addition, the inspector observed the Refueling Water Storage Tank level
              licensee obtaining samples from the warehouses and assured that                     I
instrument loops on both units. Minor insulation damage was noted on Loop
              appropriate f asteners were selected and properly identified to assure               j
No. 2FWLT 5010.
              traceability.
The licensee was informed of this damage.
            No violations or deviations were identified.                                           l
No violations or deviations were identified.
                                                                                                  J
12.
        13.   Review of Licensee Quality Assurance Performance Assessment (35701)                 ;
Followup of Compliance Bulletin 87-02, Fastener Testing to Determine
              The inspector discussed the licensee's Quality Assurance Performance                 ,
Conformance with Applicable Material Specifications (25026)
            Assessment program with licensee Quality Assurance (QA) management
j
                                                                  '
The inspectors reviewed the licensee selection process for fasteners to be
                                                                                                    \
)
                                                                                                  l
tested as required by the Bulletin.
                                                                                        -
The inspectors also observed the
                                                                                                  1
!
                                                                                                  1
licensee obtaining
samples from the warehouses and assured that
I
appropriate f asteners were selected and properly identified to assure
j
traceability.
No violations or deviations were identified.
J
13.
Review of Licensee Quality Assurance Performance Assessment (35701)
The inspector discussed the licensee's Quality Assurance Performance
,
Assessment program with licensee Quality Assurance (QA) management
'
\\
l
-
1
1


                          _
_
  .
.
                                    9
9
personnel. The licensee has implemented periodic assessments to provide
personnel.
The licensee has implemented periodic assessments to provide
nanagement awareness of the performance of their QA program and to serve
nanagement awareness of the performance of their QA program and to serve
as an input to planning the most effective use of QA resources for
as an input to planning the most effective use of QA resources for
activities such as audits and surveillances. The assessments were
activities such as audits and surveillances.
The assessments were
conceptualized in early 1987 and two assessments have been completed and
conceptualized in early 1987 and two assessments have been completed and
reports issued for the Catawba Station to date.         The reviews were
reports issued for the Catawba Station to date.
The reviews were
performed by a board composed of five members from the QA Department.
performed by a board composed of five members from the QA Department.
Various functional areas were evaluated for Central Construction and
Various functional areas were evaluated for Central Construction and
Maintenance Department and Nuclear Production Department at Catawba for
Maintenance Department and Nuclear Production Department at Catawba for
the period of January 1,1986 through May 1,1987. Input data included QA
the period of January 1,1986 through May 1,1987.
Input data included QA
Audit Deports, QA Surveillance Reports, Trend Reports, Nonconforming Item
Audit Deports, QA Surveillance Reports, Trend Reports, Nonconforming Item
Reports, Problem Investigation Reports and Incident Reports. The scensee
Reports, Problem Investigation Reports and Incident Reports. The
scensee
rated each functional area as requiring less, the same or more ottention
rated each functional area as requiring less, the same or more ottention
and shared the Catawba results with the inspector. The inspector had
and shared the Catawba results with the inspector.
The inspector had
previously expressed a concern that actual problems ought to be used to
previously expressed a concern that actual problems ought to be used to
help drive the QA audit / surveillance process. This program appears to be
help drive the QA audit / surveillance process. This program appears to be
a viable approach to that concern.
a viable approach to that concern.
No violations or deviations were identified.
No violations or deviations were identified.
                                                                          _
_
}}
}}

Latest revision as of 13:21, 11 December 2024

Insp Repts 50-413/87-42 & 50-414/87-42 on 871126-1225. Violations Noted.Major Areas Inspected:Reviews of Plant Operations,Surveilance & Maint Observations,Cold Weather Preparation & Followup of Compliance Bulletin 87-002
ML20147D090
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 01/06/1988
From: Lesser M, Peebles T, Van Doorn P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20147D004 List:
References
50-413-87-42, 50-414-87-42, IEB-87-002, IEB-87-2, NUDOCS 8801200056
Download: ML20147D090 (10)


See also: IR 05000413/1987042

Text

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UNITED STATEc

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NUCLEAP REGULATORY COMMISSION

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REGION 11

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101 MARIETTA STREET.N.W.

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ATLANTA, GEORGI A 30323

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$

...

.

Report Nos.

50-413/87-42 and 50-414/87-42

Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C.

28242

Docket Nos.:

50-413 and 50-414

License Nos.: NPF-35 and NPF-52

Facility Name: Catcwba 1 and 2

Inspection Conducted: November 26, 1987 - December 25, 1987

/

7

Inspector:

K K 'Va'n Doorn

/

D(ts/5igned

~

Inspector:)f)?// J Jh W K 5" L&'sser'~ MtVSignid /' g - M Approved by:

7 T. A. P4ebles, Section Chief Date Signed Pr jacts Branch 3 Division of Reactor Projects SUMMARY Scope: This routine, unannounced inspection was conoucted on site inspecting- in the areas of review of plant operations; surveillv e.e observatior.; maintenance observation; review of licensee nonroutine event reports; followup of previou ly identifiad items; refueling activities (Unit 1); cold weather oreparatio.s; followup of Compliance Bulletin 87-02 and review of QA performance assessment. Results: Of the nine (9) areas inspected, one apparent violation was identif f id in one area. (Failure to Properly Classify and Report a Diesel Generator Invalid Failure paragraph 6.c.) . . P P J 8801200056 8G0111 PDR ADOCK 05000413 G PDR - - . .. . - . - . ... . . . . . . . . . . - - - - . . . . - -

. -. . _- . - - . . .- .= - . - . . 1 . .. - , . . REP 0D.T DETAILS 1. Persons Contacted 'icensee Employees _

  • H. B. Barron, Operations Superintendent

< W. F. Beaver; Performance Engineer W. H. Bradley, QA Surveillance S. Brown, Reactor Engineer ' B. F. Caldwell,. Station Services Superintende t

  • R. N. Casler, Operating Engineer

R. H. Charest, Station Chemistry Supervisor

  • M. A. Cote, ' Licensing Specialist
  • T. E. Crawford, Integrated Scheduling Superintendent

W. P. Deal, Health Physics Supervisor C. S. Gregory, I. & E. Support Engineer . .,

  • J. W. Hampton, Station Manager

C. L. Hartzell, Compliance Engineer J. Knuti, Operating Engineer F. N. Mack, Project Services Engineer W. W. McCollough, Mechanical Maintenance Supervisce C. E. Muse, Oper&+ing Engineer -l T. B. Owen, Assistant Station Manager F. P. Schiff'ay, II, L~ censing Er.gineer

  • G. T. Smith, Maintenance Superintendent

J. Stackley, I. & E. Ergineer D. Tower, Shift Operating Engineer

  • R. F. Wardell, Technical Services Superintendent

' J. W. Willis, Senior QA Engineer, Operations Other licensee employees contacted included technicians, operators, ) " mechanics, security force members, and office personnel.

)

2. Exit laterview ] H Tra inspection scope and findings were summarized on December 23, 1981, with those persons indicated in paragraph 1 above. The inspector described the areas inspected and discussed in detail the inspection findings. Dissenting comments were not received from the licensee. ' ' Proprietary information is net contained in this report. The folicwing new items were identified: 1 Unresolved Item 413/87-42-01: C'osed KC Supply Valve to RHR V ichanger . in Service. Violation 413/87-42-02: Failure to Properly Classify and Repo- Diesel. . Generator Invalid Failure. ' i - - - . . , , - - - ,- .- ..a.- .. - . - ,

. - . . . . .- - .- . . . - . - . '2 . Unresolved. Item 413/87-42-03: . Inadequate Test Procedure for Blackout- Testing During Solid Plant Operations. 3. Licensee Action on Previous Enforcement _ Matters (92702) a. (CLOSED) Unresolved Item 413,414/87-05-01: Management Review ano , , Corrective Action of Excessive Problems Occurring on a Specific ' Assigned Shift. The licensee has counseled appropriate personnel and the Snift Supervisor has implemented improvements in communications on shift. The inspe tors have regu'larly observed this shif t crew and have not observed any additional significant . problems. Therefore, this item is closed. b. (CLOSED) Unresolved Itna 413/87-36-04: Icability of PORV's to Fail Scfe Clocod. NRC:RII personnel reviewed the licensee's "operability detarmination" of, the Pressurizer PORV's and found it to be accep;Tble. The licensee additior,sily was able to -correct problems with the valves and meet required stroke times under "fail safe" conditions. Based on thin the item is closed. No violations or dev. .t.ons .-ere ideatified. 4. Unresolved items * hew unresolved items are' identified in paragraphs 5.b. and 6.d. 5. Plant Operations Review (71707 c.nd 71710) a. The inspectors reviewed plant cperations throughout the reportin'g > period to verify ccnformance with regulatory *equirements, ' Technical Specifications (TS), and administrative controls. Control recm logs, danger tag logs, Technical Specification Action Item Log, and the , removal and restoration log were routinely reviewed. Shift turnovers were observed to verify that they were conducted in accordance with approved procedures. , . i The inspectors. verified by observation and interviews,-that measures - taken to a ssure physical protection of the facility met current . ; requiremen Areas inspected included the security organization, , the estahl ,,iment and maintenances of gates, r.;c-s, and isolation ' . zones in the proper condition, that access cc xc1 and badging were - proper and procedures followed. j "

  • An Unresolved Item is a matter which more information is required to dete?_

, mined whether it is acceptable or may involve a violation or deviation. , 9 ? , , - - , ,, ..,-- - - - - , ,, --,,,,nw r- c , , , , , , . , , , . , ,. - - , , ,,, , , - - . .

..y . .. .. ._ _ _. . - _ _ _ __ . - . 3- In addition to the areas discussed above, .tl , areas toured were observed for fire prevention and protection activities. These included such things-as combustible. material control, fire protection systems ~ and materials,; and-. fire protection associated with , maintenance activities. The inspectors -reviewed Problem Investigation Reports (PIRs) to . determine if - the licensee was appropriately documenting problems and implementing appropriate corrective actions. b. The inspectors conducted t. detailed walkdown.of tFe Unit 1 component cooling system and the Unit 2 Diesel Generator. A and B train electrical switchgear. The following discreparcies were noted and ! forwarded to the licensee for followup correction: The - terminal box on Limitorque operator for 1KC-2B was missing a drain plug and tarminal box covers screws were either loose or missing from 1KC-2B and 1KC-1A. It was also noted that IKC-81B, KC Supply Valve to IB Residual Heat Removal (ND) Heat Exchanger, was shut although B train ND was in service per T.S. 3.4.1.4.1. for decay heat removal. 0P/1/A/6200/04, Residual Heat Removal System, requires this valve to be open. The inspectors were told that it was closed because the NU throttle valve, was not functioning properly, allowing ~ excessive ND to flow through the heat exchanger, and 1KC-818. leaked by enough wh'~ fully closed suen that it could be closed to reduce cooling f' The inspectors noted TC flow through the heat exchanger to be approx- imately 1300 gpm with 1KC-510 closed. The inspectors were also. told that there had not been a work request initiated on 1KC-81B,-nor was there a Restoration and Removal record or an op.en item associated with the valve. The liceasee was asked.to review its procedures for edequacy of requirements to ensure proper authorization is obtained and reccrds are maintained when a valve is placed in a position other than that stated by the procedure. This is identified as Unresolved item 413/87-42-01 Closod KC Supply Valve to RHR Heat Exchanger in Service, pending NRC and licensee review of prc:edural adequacy to maintain control over valve positions. c. Unit 2 Summary 7 The Unit started the reporting period at 75% power,. coasting down in- prepa*atior. for first refueling outage which was scheduled to commence December 18. Due to delays in the Unit refueling, it was determined to extend Unit 2 operation for 5 extra days and power was reduced to 65%. Unit 2 shutdown to commence its first refueling outage on December 23. No violations or deviattor.s were identified. 'l Y r . , ~ , . _ . .,,_. . - . . , - _ , ,, , _ .. ~-, m,...- . . - - , ~ .

. - - . - _. - _. . . . . 4 6. Surveillance Observation (61726) a. During the inspection period, the inspector verified plant operations were in compliance with various TS requirements. Typical of these requirements were confirmation of compliance with the TS for reactor coolant chemistry, refueling water _ tank, emergency - power- systems, safety injection, emergency safeguards systems,, control room- ventilation, and direct current electrical power sources. The inspector verified that surveillance testing lwas performed in accordance with'the approved written procedures, test instrumentation was calibrated, limiting conditions for operation were met, appro- priate removal and restoration of the affected equipment- was accomplished, test results met requirements and were reviewed by personnel other than the individual directing the test, and that any deficiencies identified during the testing were properly reviewed and resolved by appropriate management personnel. b. The following surveillance activity was witnessed: PT/1/A/4200/09 Train B Safety Injection, Phase'A, Phase B, and Blackout Testing. c. On November 13, 1987 the 1A Diesel Generator tripped after start number 548 due to the P-3 shuttle valve failing to seat properly. , l This valve vents control air pressure on emergency trip signals to - shutdown the engine. Operations Management Procedure- (OMP) 2-28. Diesel Generator Logbook, requires tuat each diesel generator start attempt be classified as a Valid Success / Failure or Invalid Test / Failure. The licensee failed to properly classify the trip as an _ invalid failure until prompted by the' NRC resident inspectors. Following discussions with the licensee personnel, an intrastation , letter dated December 9,1987 from R.N. Casler to Lee Hartzell was issued which reclassified the trip from an invalid test to an invalid failure. Consequently the itcensee failed to report the diesel generator failure to the NRC within 30 days per T.S. 4.8.1.1.3. This constitutes a violation of T.S. 4.8.1.1. 3 and 6.8.1. Violation 413/87-42-02: Failure to Properly Classify and Report a Diesel Generator Invalid Failure. The resident inspectors reviewed the Diesel Generator Logbooks as part of this investigation and noted numerous errors indicating that increased attention is necessary in tracking and evaluating diesel , starts. The Test Failure / Invalid Test Description Sheet for the IB ' diesel generator valid failure on start number 719 had not been initiated. As of December 18, Description Sheets for starts 718-751 j on the 18 diesci generator, done between December 1-5, had not been reviewed by the Unit Coordinator or his designee and approximately 4 i of these starts had not been reviewed by the Shift or Unit 1 i 5-

. . 5 Supervisor. OMP 2-29 requires these reviews to be completed within seven days. Finally the index of the logbook had two separate starts on different dates identified as start number 718. The licensee acknowledged weaknesses in this area and agreed that increased supervisory attention is required. The inspectors also held discussions with the licensee to clarify the reportability and classification requirements of Regulatory Guide 1.108 Rev.1, Periodic Testing of Diesel Generator Units as Onsite Electric Power Systems at Nuclear Plants. The licensee agreed to revise OMP 2-28 to ensure specifically that diesel generator valid and invalid failures were properly classified and reported. d. On December 3, 1987 "B" train blackout ESF testing was being conducted on Unit I while the plant was solid. Reactor Coolant (NC) System pressure was being maintained at approximately 325 psig. Both trains of Component Cooling (KC) were supplying the "A" train Residual Heat Removal (ND) heat exchanger. Upon initiating a blackout signal on "B" train 4160 KV bus, B train KC pumps were de-energized until the IB diesel generator started and sequenced on the pumps. The partial loss of KC caused the NC system to heat up slightly, however since the plant was solid a large pressure increase occurred and resulted in the pressurizer power operated relief valve (PORV) setting of 400 psig being exceeded. One PORV opened to relieve the pressure. The testing was initially intended to be performed when the plant was not solid however problems with equipment forced a delay. Apparently the consequences of losing one train of KC while solid were inadequately evaluated prior to approvhl of the test. This is identified as Unresolved Item 413/87-42-03: Inadequate Test Procedure for Blackout Testing During Solid Plant Operations, pending further review by the inspectors. Cne violation was identified as described in paragraph 6.c. above. 7. Maintenance Observations (62703) a. Station maintenance activities of selected systems and components were observed / reviewed to ascertain that they were conducted in accordance with requirements. The inspector verified licensee conformance to the requirements in the following areas of inspection: the activities were accomplished using approved procedures, and functional testing and/or calibrations were performed prior to returning components or systems to service; quality control records were maintained; activities performed were accomplished by qualified personnel; and materials used were properly certified. Work requests were reviewed to determine status of outstanding jobs and to assure that priority is assioned to safety-related equipment maintenance which may effect systam performance.

. _ _ _ _. . . .

6 1 b. The inspector witnessed portions of. the 'following maintenance activity in progress: PT/1/A/4200/23A -Post Maintenance Stroke Timing of.PORV 1NC-34A_ No violations or deviations were identified. 8. Review of Licensee Nonroutine Event Reports ~(92700) a. The below listed Licensee Event Reports (LER) were' reviewed to determine if the information provided met NRC requirements. .The determination included: adequacy of description, verification of compliance with Technical Specifications and regulatory requirements, corrective action taken, existence of potential generic problems, reporting requirements satisfied, and the relative- safety significance of each -event. Additional implant reviews and discussion with plant personnel, as appropriate, were conducted for those reports indicated by an (*). The following LERs are closed: , '

  • 413/85-53 Rv.1

Diesel Generator IA Battery Charger Inoperable Due to Blown Fuses

  • 413/86-58 Rv.1

Reactor Trip and Feedwater Isolation Due to an Unexpected Response from RTD Simulator 413/87-38 Missed Hourly Fire Watches Result in TS Violation Due to a Personnel Error !

  • 413/87-40

Turbine Driven Auxiliary Feedwater Pump Auto-Start Signal / Steam Generator Blowdown Containment Isolation Valves Actuation Due to Procedural Deficiency

  • 414/87-07 Rv.1

Reactor Trip Due to a Management Deficiency and Equipment Failures b. On November 5, 1987 with Unit 2 in Mode 4, a Main Feedwater (CF) Isolation and an Auxiliary Feedwater (CA) Auto Start occurred when IAE technicians shut the root valve for Steam Generator 2C Narrow Range level Channel IV instead of Channel II. When the line was vented the 2/4 logic for Hi Hi Steam Generator level was made up. This incident is described in LER 414/87-30. The root cause of the event is an apparent personnel error in that the technicians did not properly identify the correct component. The technicians however; were severely hampered by inadequate root valve labeling and 1 instrument detail drawings that are vague, cluttered and difficult to_ ' comprehend. A Station Problem Report has been initiated to review a steam generator level channel drawings and the licensee intends to ' i effectively label steam generator and pressurizer instrument valves. , f

- . . - - . .. .. . -. . _ . .- .. ._._

_ . _ . . . _ _. - _ _ _ _ _ . _ . . ' ' .' 7 These same' problems with instrument' labeling and detail drawings . possibly go beyond the steam generators and pressurizer. The Duke Power Labeling Committee has been established to label plant- components and. valves. This LER remains open pending further review by the inspectors.into the personnel error and the labeling program. c. LER 413/87-39 discussed ' corrective action for a spurious CA auto-start due to the ' simultaneous implementation of 2 Nuclear Station' Modifications (NSM). The corrective action includes- adding information to test procedures which state that CA auto-start will occur if an auto-start signal is received due to other maintenance activities in progress while Solid State Protection System (SSPS) is in test. The LER further states that these procedure changes will make CA auto-starts, under these conditions, not reportable. The inspectors informed the licensee that 10CFR 50.73 and NUREG 1022 clearly does not exempt these spurious ESFs from being reportable unless the licensee can show that the actuation was part of a preplanned sequence during testing or operation. The licensee was asked to ensure this policy'is clearly understood by its personnel. The licensee was also informed that since the wording in the LER might imply otherwise, it would be appropriate to submit a supple- mented LER elaborating on the corrective actions. No violations or deviations were identified. 9. Refueling Activities and Startup After Refueling (Unit 1) (60710 & 71711) a. The inspectors verified that T.S. applicable to Modes 4, 5, and 6 were met, reactor coolant level control practices were followed, containment cleanliness inspections and cleanup was adequate and procedures were in use ensure systems disturbed or tested during the outage were returned to operable status. - b. Unit 2 Summary The unit completed containment Intergrated Leak Rate Test i successfully on November 25. The test was witnessed by the resident and regional inspectors. The unit also entered Mode 5 on November 1 25. On December 10 a borated water leak of 1-2 gpm was discovered on a Control Rod Drive Mechanism (CRDM) Vent plug. The leak had been in existence for 24-36 hours and spilled borated water on the vessel head and wetted CRDM cabling and rod position indication cabling. An extensive cleanup effort was required which included removal of boron crystals and drying out and testing electrical cabling. To perform this the outage had to be extended an additional two weeks. Concurrently with discovering the vent plug leak the licensee discovered evidence to indicate a small primary to secondary leak in the 1A Steam Generator. Efforts to locate the leaking tube included i ..- - l

. - - . _ - . .- .. , . . 8 pressurizing .the tscondary. side to 800 psig and inspecting for' tube in leakage, however were unsuccessful. The licensee estimated the , leak rate to be 17 gallons per day from detected activity levels in the secondary. The resident inspectors will' closely monitor licensee activities to better quantify the leak during startup. The unit entered Mode 4 on' December 22 and Mode 3 on December 23. No violations or deviations were identified. 10. Previously Identified Inspector Findings (92701) (CLOSED) Inspector Followup Item 87-07-01: Failure to Demonstrate Adequate Access Control Measures, for the OSC as Stated in Exercise Objective B.1.K. The . licensee has determined that the objective was inappropriate for the exercise since the.0SC is inside the protected area. In addition the OSC Coordinator has been charged with controlling any access problems and has the authority to have personnel removed. Licensee actions are acceptable. No violations or deviations were identified. 11. Cold Weather Preparations (71714) The inspectors verified that the licensee was inspecting / repairing cold weather protection devices in preparation for the winter season. Work Request 3057 SWR for inspection of thermostats, heaters and. instrumen- tation boxes had been implemented. Additional Work Requests 8601 IAE and 8606 IAE were issued to complete required repairs. The inspector reviewed documentation on the Work Requests which showed that all repairs had been made except for- replacement of some rusted screws on one heater box. In addition, the inspector observed the Refueling Water Storage Tank level instrument loops on both units. Minor insulation damage was noted on Loop No. 2FWLT 5010. The licensee was informed of this damage. No violations or deviations were identified. 12. Followup of Compliance Bulletin 87-02, Fastener Testing to Determine Conformance with Applicable Material Specifications (25026) j The inspectors reviewed the licensee selection process for fasteners to be ) tested as required by the Bulletin. The inspectors also observed the ! licensee obtaining samples from the warehouses and assured that I appropriate f asteners were selected and properly identified to assure j traceability. No violations or deviations were identified. J 13. Review of Licensee Quality Assurance Performance Assessment (35701) The inspector discussed the licensee's Quality Assurance Performance , Assessment program with licensee Quality Assurance (QA) management ' \\ l - 1 1

_ . 9 personnel. The licensee has implemented periodic assessments to provide nanagement awareness of the performance of their QA program and to serve as an input to planning the most effective use of QA resources for activities such as audits and surveillances. The assessments were conceptualized in early 1987 and two assessments have been completed and reports issued for the Catawba Station to date. The reviews were performed by a board composed of five members from the QA Department. Various functional areas were evaluated for Central Construction and Maintenance Department and Nuclear Production Department at Catawba for the period of January 1,1986 through May 1,1987. Input data included QA Audit Deports, QA Surveillance Reports, Trend Reports, Nonconforming Item Reports, Problem Investigation Reports and Incident Reports. The scensee rated each functional area as requiring less, the same or more ottention and shared the Catawba results with the inspector. The inspector had previously expressed a concern that actual problems ought to be used to help drive the QA audit / surveillance process. This program appears to be a viable approach to that concern. No violations or deviations were identified. _ }}