IR 05000271/2006003: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:July 26, 2006 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Raymond J. Powell, Chief Projects Branch 5 Division of Reactor Projects Enclosure | Raymond J. Powell, Chief Projects Branch 5 Division of Reactor Projects | ||
Enclosure | |||
cc w/encl: | cc w/encl: | ||
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J. E. Silberg, Pillsbury, Winthrop, Shaw, Pittman LLP G. D. Bisbee, Esquire, Deputy Attorney General, Environmental Protection Bureau J. Block, Esquire J. P. Matteau, Executive Director, Windham Regional Commission D. Katz, Citizens Awareness Network (CAN) | J. E. Silberg, Pillsbury, Winthrop, Shaw, Pittman LLP G. D. Bisbee, Esquire, Deputy Attorney General, Environmental Protection Bureau J. Block, Esquire J. P. Matteau, Executive Director, Windham Regional Commission D. Katz, Citizens Awareness Network (CAN) | ||
R. Shadis, New England Coalition Staff G. Sachs, President/Staff Person, c/o Stopthesale C. McCombs, Director, Commonwealth of Massachusetts, SLO Designee State of New Hampshire, SLO Designee State of Vermont, SLO Designee | R. Shadis, New England Coalition Staff G. Sachs, President/Staff Person, c/o Stopthesale C. McCombs, Director, Commonwealth of Massachusetts, SLO Designee State of New Hampshire, SLO Designee State of Vermont, SLO Designee | ||
Enclosure | |||
Distribution w/encl: | Distribution w/encl: | ||
S. Collins, RA M. Dapas, DRA R. Powell, DRP T. Walker, DRP B. Sosa, RI OEDO D. Roberts, NRR R. Ennis, EPU PM, NRR R. Laufer, NRR J. Shea, PM, NRR T. Tate, Backup PM, NRR D. Pelton, DRP, Senior Resident Inspector A. Rancourt, DRP, Resident OA Region I Docket Room (with concurrences) | S. Collins, RA M. Dapas, DRA R. Powell, DRP T. Walker, DRP B. Sosa, RI OEDO D. Roberts, NRR R. Ennis, EPU PM, NRR R. Laufer, NRR J. Shea, PM, NRR T. Tate, Backup PM, NRR D. Pelton, DRP, Senior Resident Inspector A. Rancourt, DRP, Resident OA Region I Docket Room (with concurrences) | ||
ROPreports@nrc.gov (All IRs) | ROPreports@nrc.gov (All IRs) | ||
C:\My Files\Copies\VY IR 2006-03REV1.wpd SUNSI Review Complete: TEW | C:\\My Files\\Copies\\VY IR 2006-03REV1.wpd SUNSI Review Complete: TEW (Reviewers Initials) | ||
After declaring this document An Official Agency Record it will be released to the Public. | After declaring this document An Official Agency Record it will be released to the Public. | ||
To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RI/DRP | To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RI/DRP RI/DRP RI/DRP NAME DPelton/BES for TWalker RPowell DATE 07/24/06 07/24/06 07/26/06 OFFICIAL RECORD COPY | ||
Enclosure i | |||
U.S. NUCLEAR REGULATORY COMMISSION | U.S. NUCLEAR REGULATORY COMMISSION | ||
==REGION I== | ==REGION I== | ||
Docket No.: 50-271 Licensee No.: DPR-28 Report No.: 05000271/2006003 Licensee: Entergy Nuclear Operations, Inc. | Docket No.: | ||
50-271 Licensee No.: | |||
DPR-28 Report No.: | |||
05000271/2006003 Licensee: | |||
Entergy Nuclear Operations, Inc. | |||
Facility: | |||
Vermont Yankee Nuclear Power Station Location: | |||
320 Governor Hunt Road Vernon, Vermont 05354-9766 Dates: | |||
April 1, 2006 through June 30, 2006 Inspectors: | |||
David L. Pelton, VY Senior Resident Inspector Beth E. Sienel, VY Resident Inspector Tracy E. Walker, Senior Project Engineer Jennifer A. Bobiak, Reactor Inspector, DRS Patrick W. Finney, Reactor Inspector, DRS James D. Noggle, Senior Health Physicist, DRS Approved by: | |||
Raymond J. Powell, Chief Projects Branch 5 Division of Reactor Projects | |||
Enclosure ii | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
| Line 77: | Line 93: | ||
===NRC-Identified and Self-Revealing Findings=== | ===NRC-Identified and Self-Revealing Findings=== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
B | B. | ||
Licensee Identified Findings None. | |||
=REPORT DETAILS= | =REPORT DETAILS= | ||
===Summary of Plant Status=== | ===Summary of Plant Status=== | ||
Vermont Yankee (VY) Nuclear Power Station began the inspection period operating at 87% | Vermont Yankee (VY) Nuclear Power Station began the inspection period operating at 87% | ||
reactor power. At that time, Entergy personnel were performing power ascension testing activities related to an NRC license amendment authorizing an increase in VYs licensed maximum reactor power level from 1593 megawatts thermal (MWth) to 1912 MWth. On April 1, operators increase power to approximately 91%. Power was again increased to approximately 93% and 96% on April 6 and 22, respectively. On April 28, power was increased to 98%. | reactor power. At that time, Entergy personnel were performing power ascension testing activities related to an NRC license amendment authorizing an increase in VYs licensed maximum reactor power level from 1593 megawatts thermal (MWth) to 1912 MWth. On April 1, operators increase power to approximately 91%. Power was again increased to approximately 93% and 96% on April 6 and 22, respectively. On April 28, power was increased to 98%. | ||
| Line 101: | Line 115: | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity {{a|1R01}} | Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity {{a|1R01}} | ||
==1R01 Adverse Weather Protection== | ==1R01 Adverse Weather Protection== | ||
{{IP sample|IP=IP 71111.01}} | {{IP sample|IP=IP 71111.01}} | ||
===.1 Readiness for Seasonal Susceptibilities=== | ===.1 Readiness for Seasonal Susceptibilities=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
(one sample) | (one sample) | ||
| Line 111: | Line 126: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R04}} | No findings of significance were identified. {{a|1R04}} | ||
==1R04 Equipment Alignment== | ==1R04 Equipment Alignment== | ||
{{IP sample|IP=IP 71111.04}} | {{IP sample|IP=IP 71111.04}} | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R05}} | No findings of significance were identified. {{a|1R05}} | ||
==1R05 Fire Protection== | ==1R05 Fire Protection== | ||
{{IP sample|IP=IP 71111.05Q}} | {{IP sample|IP=IP 71111.05Q}} | ||
| Line 143: | Line 160: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R06}} | No findings of significance were identified. {{a|1R06}} | ||
==1R06 Flood Protection Measures== | ==1R06 Flood Protection Measures== | ||
{{IP sample|IP=IP 71111.06}} | {{IP sample|IP=IP 71111.06}} | ||
| Line 152: | Line 170: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R07}} | No findings of significance were identified. {{a|1R07}} | ||
==1R07 Heat Sink Performance== | ==1R07 Heat Sink Performance== | ||
{{IP sample|IP=IP 71111.07}} | {{IP sample|IP=IP 71111.07}} | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R11}} | No findings of significance were identified. {{a|1R11}} | ||
==1R11 Licensed Operator Requalification== | ==1R11 Licensed Operator Requalification== | ||
{{IP sample|IP=IP 71111.11Q}} | {{IP sample|IP=IP 71111.11Q}} | ||
| Line 176: | Line 196: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R12}} | No findings of significance were identified. {{a|1R12}} | ||
==1R12 Maintenance Effectiveness== | ==1R12 Maintenance Effectiveness== | ||
{{IP sample|IP=IP 71111.12Q}} | {{IP sample|IP=IP 71111.12Q}} | ||
| Line 185: | Line 206: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R13}} | No findings of significance were identified. {{a|1R13}} | ||
==1R13 Maintenance Risk Assessment and Emergent Work Evaluation== | ==1R13 Maintenance Risk Assessment and Emergent Work Evaluation== | ||
{{IP sample|IP=IP 71111.13}} | {{IP sample|IP=IP 71111.13}} | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R14}} | No findings of significance were identified. {{a|1R14}} | ||
==1R14 Personnel Performance During Non-Routine Plant Evolutions== | ==1R14 Personnel Performance During Non-Routine Plant Evolutions== | ||
{{IP sample|IP=IP 71111.14}} | {{IP sample|IP=IP 71111.14}} | ||
| Line 212: | Line 235: | ||
This 5% increase was broken into two separate 2.5% reactor power increases, performed on April 6 and April 22. The increase was performed in two increments due to a hold that had been temporarily placed on EPU testing. | This 5% increase was broken into two separate 2.5% reactor power increases, performed on April 6 and April 22. The increase was performed in two increments due to a hold that had been temporarily placed on EPU testing. | ||
(See Section 4OA5.1 of this report for more detail.); and | |||
* The fourth of four planned 5% reactor power increases in support of EPU. This 5% increase was also broken into two separate 2.5% reactor power increases, performed on April 28 and May 5. The increase was performed in two increments due to two holds that had been placed on EPU testing. | * The fourth of four planned 5% reactor power increases in support of EPU. This 5% increase was also broken into two separate 2.5% reactor power increases, performed on April 28 and May 5. The increase was performed in two increments due to two holds that had been placed on EPU testing. | ||
(See Section 4OA5.1 of this report for more detail). | |||
The adequacy of personnel performance, procedure compliance, and use of the corrective action process for all non-routine evolutions were evaluated against the requirements and expectations contained in TS and the following station procedures, as applicable: | The adequacy of personnel performance, procedure compliance, and use of the corrective action process for all non-routine evolutions were evaluated against the requirements and expectations contained in TS and the following station procedures, as applicable: | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R15}} | No findings of significance were identified. {{a|1R15}} | ||
==1R15 Operability Evaluations== | ==1R15 Operability Evaluations== | ||
{{IP sample|IP=IP 71111.15}} | {{IP sample|IP=IP 71111.15}} | ||
| Line 244: | Line 268: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R19}} | No findings of significance were identified. {{a|1R19}} | ||
==1R19 Post Maintenance Testing== | ==1R19 Post Maintenance Testing== | ||
{{IP sample|IP=IP 71111.19}} | {{IP sample|IP=IP 71111.19}} | ||
| Line 258: | Line 283: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R22}} | No findings of significance were identified. {{a|1R22}} | ||
==1R22 Surveillance Testing== | ==1R22 Surveillance Testing== | ||
{{IP sample|IP=IP 71111.22}} | {{IP sample|IP=IP 71111.22}} | ||
| Line 274: | Line 300: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R23}} | No findings of significance were identified. {{a|1R23}} | ||
==1R23 Temporary Plant Modifications== | ==1R23 Temporary Plant Modifications== | ||
{{IP sample|IP=IP 71111.23}} | {{IP sample|IP=IP 71111.23}} | ||
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==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
===Cornerstone: Public Radiation Safety=== | ===Cornerstone: Public Radiation Safety=== | ||
2PS3 Radiological Environmental Monitoring Program (REMP) (71122.03) | 2PS3 Radiological Environmental Monitoring Program (REMP) (71122.03) | ||
| Line 303: | Line 328: | ||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
{{a|4OA1}} | {{a|4OA1}} | ||
==4OA1 Performance Indicator Verification== | ==4OA1 Performance Indicator Verification== | ||
{{IP sample|IP=IP 71151}} | {{IP sample|IP=IP 71151}} | ||
| Line 318: | Line 344: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|4OA2}} | No findings of significance were identified. {{a|4OA2}} | ||
==4OA2 Identification and Resolution of Problems== | ==4OA2 Identification and Resolution of Problems== | ||
{{IP sample|IP=IP 71152}} | {{IP sample|IP=IP 71152}} | ||
===.1 Review of Items Entered into the Corrective Action Program=== | ===.1 Review of Items Entered into the Corrective Action Program=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into Entergys corrective action program at an appropriate threshold and that adequate attention was being given to timely corrective actions. Additionally, in order to identify repetitive equipment failures and/or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into Entergys corrective action program. This review was accomplished by reviewing the description of each new CR and/or by attending daily CR screening meetings. A listing of CRs and other documents reviewed is included in the attachment to this report. | The inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into Entergys corrective action program at an appropriate threshold and that adequate attention was being given to timely corrective actions. Additionally, in order to identify repetitive equipment failures and/or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into Entergys corrective action program. This review was accomplished by reviewing the description of each new CR and/or by attending daily CR screening meetings. A listing of CRs and other documents reviewed is included in the attachment to this report. | ||
b. Assessments and Observations No findings of significance were identified. | b. | ||
Assessments and Observations No findings of significance were identified. | |||
===.2 Semi-Annual Trend Review=== | ===.2 Semi-Annual Trend Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review of Entergys corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The review was focused on human performance-related issues and considered the results of reviews discussed in Section 4OA2.1. The inspectors review nominally considered the six-month period of January through June 2006. The inspectors compared their results with the results contained in Entergys quarterly trend report for the first quarter 2006; recently developed trend condition reports; Entergys human performance PI data; and discussions with Operations, Radiation Protection (RP), and Technical Support Department management. The corrective actions assigned to address the individual issues as well as to address human performance trends were reviewed for adequacy. | The inspectors performed a review of Entergys corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The review was focused on human performance-related issues and considered the results of reviews discussed in Section 4OA2.1. The inspectors review nominally considered the six-month period of January through June 2006. The inspectors compared their results with the results contained in Entergys quarterly trend report for the first quarter 2006; recently developed trend condition reports; Entergys human performance PI data; and discussions with Operations, Radiation Protection (RP), and Technical Support Department management. The corrective actions assigned to address the individual issues as well as to address human performance trends were reviewed for adequacy. | ||
b. Assessment and Observations No findings of significance were identified. | b. | ||
Assessment and Observations No findings of significance were identified. | |||
In May 2006, the Operations Manager initiated trending CR 2006-1492 that summarized two recent Operations Department human performance errors. These errors included operator manipulation of an incorrect valve while attempting to remove the C condensate demineralizer from service and an operator inadvertently tripping open a breaker associated with the EDGs while hanging a tag on an adjacent breaker. As a result of these errors, the Operations Department Human Performance PI turned Red. | In May 2006, the Operations Manager initiated trending CR 2006-1492 that summarized two recent Operations Department human performance errors. These errors included operator manipulation of an incorrect valve while attempting to remove the C condensate demineralizer from service and an operator inadvertently tripping open a breaker associated with the EDGs while hanging a tag on an adjacent breaker. As a result of these errors, the Operations Department Human Performance PI turned Red. | ||
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===.3 Annual Sample Review - Special Nuclear Material Controls=== | ===.3 Annual Sample Review - Special Nuclear Material Controls=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
(one sample) | (one sample) | ||
| Line 364: | Line 393: | ||
===.4 Annual Sample: Failure of Emergency Diesel Generator Loss of Field Relays=== | ===.4 Annual Sample: Failure of Emergency Diesel Generator Loss of Field Relays=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
(one sample) | (one sample) | ||
| Line 378: | Line 406: | ||
Entergy entered this issue into their corrective action program (CR 2006-1438) and incorporated the information into the pre-job briefing form used during monthly EDG surveillances. This finding was minor because operators had received licensed operator requalification training on the November 2005 EDG event, which included the associated operator responses, and operating procedures were in place to take appropriate emergency actions in the case of abnormal EDG performance. | Entergy entered this issue into their corrective action program (CR 2006-1438) and incorporated the information into the pre-job briefing form used during monthly EDG surveillances. This finding was minor because operators had received licensed operator requalification training on the November 2005 EDG event, which included the associated operator responses, and operating procedures were in place to take appropriate emergency actions in the case of abnormal EDG performance. | ||
{{a|4OA3}} | {{a|4OA3}} | ||
==4OA3 Event Followup== | ==4OA3 Event Followup== | ||
{{IP sample|IP=IP 71153}} | {{IP sample|IP=IP 71153}} | ||
===.1 Indications of a Fire in the East Switchgear Room and the Declaration of an Unusual=== | ===.1 Indications of a Fire in the East Switchgear Room and the Declaration of an Unusual=== | ||
Event | Event | ||
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{{a|4OA5}} | {{a|4OA5}} | ||
==4OA5 Other== | ==4OA5 Other== | ||
===.1 Power Uprate: Power Ascension Testing=== | ===.1 Power Uprate: Power Ascension Testing=== | ||
{{IP sample|IP=IP 71004}} | {{IP sample|IP=IP 71004}} | ||
| Line 425: | Line 454: | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===.2 (Closed) URI 05000271/2006002-01: Training Provided to Licensed Operators | ===.2 (Closed) URI 05000271/2006002-01:=== | ||
Training Provided to Licensed Operators Regarding Plant Response to a Condensate Pump Trip During the observation of training initially provided to licensed operators on the expected plant response to a trip of a condensate pump from 100% reactor power, the inspectors noted that the simulated plant response differed from the predicted plant response indicated in Reactor Engineerings analysis for this event. The difference was in the final values of core thermal power and core flow immediately following the pump trip. | |||
Regarding Plant Response to a Condensate Pump Trip During the observation of training initially provided to licensed operators on the expected plant response to a trip of a condensate pump from 100% reactor power, the inspectors noted that the simulated plant response differed from the predicted plant response indicated in Reactor Engineerings analysis for this event. The difference was in the final values of core thermal power and core flow immediately following the pump trip. | |||
At that time, the inspectors were concerned that the condensate pump trip training initially provided to licensed operators did not meet the met the guidance outlined in American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.5-1998, Nuclear Power Plant Simulators for Use in Operator Training and Examination. Based on the results of the inspections of licensed operator training discussed in Section 1R11 and on the results of the inspections of the condensate pump trip test discussed in Section 4OA5.1, the inspectors concluded that the condensate pump trip training provided to licensed operators met the guidance outlined in ANSI/ANS-3.5-1998. | At that time, the inspectors were concerned that the condensate pump trip training initially provided to licensed operators did not meet the met the guidance outlined in American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.5-1998, Nuclear Power Plant Simulators for Use in Operator Training and Examination. Based on the results of the inspections of licensed operator training discussed in Section 1R11 and on the results of the inspections of the condensate pump trip test discussed in Section 4OA5.1, the inspectors concluded that the condensate pump trip training provided to licensed operators met the guidance outlined in ANSI/ANS-3.5-1998. | ||
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===.3 (Closed) NRC Temporary Instruction (TI) 2515/165, Operational Readiness of Offsite=== | ===.3 (Closed) NRC Temporary Instruction (TI) 2515/165, Operational Readiness of Offsite=== | ||
Power and Impact on Plant Risk | Power and Impact on Plant Risk | ||
| Line 446: | Line 473: | ||
===.4 Institute of Nuclear Power Operations (INPO)/World Association of Nuclear Operators=== | ===.4 Institute of Nuclear Power Operations (INPO)/World Association of Nuclear Operators=== | ||
(WANO) Plant Assessment Report Review The inspectors reviewed the final report for the INPO/WANO plant assessment of the Vermont Yankee Power Station conducted in April 2005. The inspectors reviewed the report to ensure that issues identified were consistent with the NRC perspectives of Entergys performance and to verify if any significant safety issues were identified that required further NRC follow-up. | |||
{{a|4OA6}} | |||
==4OA6 Meetings, Including Exit== | ==4OA6 Meetings, Including Exit== | ||
===Exit Meeting Summary=== | ===Exit Meeting Summary=== | ||
On July 12, the resident inspectors presented the inspection results to Messrs. Bill Maguire and John Dreyfuss and members of the VY staff. The inspectors asked whether any materials examined during the inspection should be considered proprietary. | On July 12, the resident inspectors presented the inspection results to Messrs. Bill Maguire and John Dreyfuss and members of the VY staff. The inspectors asked whether any materials examined during the inspection should be considered proprietary. | ||
| Line 463: | Line 488: | ||
==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
Entergy Personnel | Entergy Personnel | ||
: [[contact::J. Devincentis]], Licensing Manager | : [[contact::J. Devincentis]], Licensing Manager | ||
: [[contact::J. Dreyfuss]], Director of Engineering | : [[contact::J. Dreyfuss]], Director of Engineering | ||
: [[contact::M. Hamer]], Licensing | : [[contact::M. Hamer]], Licensing | ||
: [[contact::W. Maguire]], General Manager of Plant Operations | : [[contact::W. Maguire]], General Manager of Plant Operations | ||
: [[contact::K. Pushee]], Radiation Protection Manager | : [[contact::K. Pushee]], Radiation Protection Manager | ||
: [[contact::N. Rademacher]], Director of Nuclear Safety | : [[contact::N. Rademacher]], Director of Nuclear Safety | ||
: [[contact::J. Thayer]], Site Vice President (former) | : [[contact::J. Thayer]], Site Vice President (former) | ||
: [[contact::T. Sullivan]], Site Vice President (current) | : [[contact::T. Sullivan]], Site Vice President (current) | ||
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED== | ==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED== | ||
===Opened=== | ===Opened=== | ||
: 05000271/2006003-01 | : 05000271/2006003-01 URI Condensate Pump Motor Fault and Switchgear Room CO2 Initiation Result in the Declaration of an Unusual Event (Section 4OA3.1) | ||
===Closed=== | ===Closed=== | ||
: 05000271/2004007-01 | : 05000271/2004007-01 VIO Did Not Keep Adequate Records, Follow Procedures, and Perform Physical Inventory of Special Nuclear Material (Section 4OA2.3) | ||
: 05000271/2005005-03 | : 05000271/2005005-03 URI Information Needed to Validate the Direct Dose Calculation Method in ODCM Section 6.11.1 (Section 2PS3) | ||
: 05000271/2006002-01 | : 05000271/2006002-01 URI Training Provided to Licensed Operators Regarding Plant Response to a Condensate Pump Trip (Section 4OA5.2) | ||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} | ||
Latest revision as of 07:49, 15 January 2025
| ML062080415 | |
| Person / Time | |
|---|---|
| Site: | Vermont Yankee File:NorthStar Vermont Yankee icon.png |
| Issue date: | 07/27/2006 |
| From: | Racquel Powell NRC/RGN-I/DRP/PB5 |
| To: | Ted Sullivan Entergy Nuclear Operations |
| References | |
| IR-06-003 | |
| Download: ML062080415 (31) | |
Text
July 26, 2006
SUBJECT:
VERMONT YANKEE NUCLEAR POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000271/2006003
Dear Mr. Sullivan:
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Vermont Yankee Nuclear Power Station. The enclosed report documents the inspection findings which were discussed on July 12, 2006, with members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the results of this inspection, no findings of significance were identified.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Raymond J. Powell, Chief Projects Branch 5 Division of Reactor Projects
Enclosure
cc w/encl:
M. R. Kansler, President, Entergy Nuclear Operations, Inc.
G. J. Taylor, Chief Executive Officer, Entergy Operations J. T. Herron, Senior Vice President and Chief Operating Officer C. Schwarz, Vice-President, Operations Support O. Limpias, Vice President, Engineering J. M. DeVincentis, Manager, Licensing, Vermont Yankee Nuclear Power Station Operating Experience Coordinator, Vermont Yankee Nuclear Power Station W. Maguire, General Manager, Plant Operations, Entergy Nuclear Operations, Inc.
N. Rademacher, Director NSA, Vermont Yankee Nuclear Power Station J. F. McCann, Director, Licensing C. D. Faison, Manager, Licensing M. J. Colomb, Director of Oversight, Entergy Nuclear Operations, Inc.
T. C. McCullough, Assistant General Counsel, Entergy Nuclear Operations, Inc.
J. H. Sniezek, PWR SRC Consultant M. D. Lyster, PWR SRC Consultant S. Lousteau, Treasury Department, Entergy Services, Inc.
Administrator, Bureau of Radiological Health, State of New Hampshire Chief, Safety Unit, Office of the Attorney General, Commonwealth of Mass.
J. E. Silberg, Pillsbury, Winthrop, Shaw, Pittman LLP G. D. Bisbee, Esquire, Deputy Attorney General, Environmental Protection Bureau J. Block, Esquire J. P. Matteau, Executive Director, Windham Regional Commission D. Katz, Citizens Awareness Network (CAN)
R. Shadis, New England Coalition Staff G. Sachs, President/Staff Person, c/o Stopthesale C. McCombs, Director, Commonwealth of Massachusetts, SLO Designee State of New Hampshire, SLO Designee State of Vermont, SLO Designee
Enclosure
Distribution w/encl:
S. Collins, RA M. Dapas, DRA R. Powell, DRP T. Walker, DRP B. Sosa, RI OEDO D. Roberts, NRR R. Ennis, EPU PM, NRR R. Laufer, NRR J. Shea, PM, NRR T. Tate, Backup PM, NRR D. Pelton, DRP, Senior Resident Inspector A. Rancourt, DRP, Resident OA Region I Docket Room (with concurrences)
ROPreports@nrc.gov (All IRs)
C:\\My Files\\Copies\\VY IR 2006-03REV1.wpd SUNSI Review Complete: TEW (Reviewers Initials)
After declaring this document An Official Agency Record it will be released to the Public.
To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RI/DRP RI/DRP RI/DRP NAME DPelton/BES for TWalker RPowell DATE 07/24/06 07/24/06 07/26/06 OFFICIAL RECORD COPY
Enclosure i
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket No.:
50-271 Licensee No.:
DPR-28 Report No.:
05000271/2006003 Licensee:
Entergy Nuclear Operations, Inc.
Facility:
Vermont Yankee Nuclear Power Station Location:
320 Governor Hunt Road Vernon, Vermont 05354-9766 Dates:
April 1, 2006 through June 30, 2006 Inspectors:
David L. Pelton, VY Senior Resident Inspector Beth E. Sienel, VY Resident Inspector Tracy E. Walker, Senior Project Engineer Jennifer A. Bobiak, Reactor Inspector, DRS Patrick W. Finney, Reactor Inspector, DRS James D. Noggle, Senior Health Physicist, DRS Approved by:
Raymond J. Powell, Chief Projects Branch 5 Division of Reactor Projects
Enclosure ii
SUMMARY OF FINDINGS
IR 05000271/2006003; 04/01/06 - 06/30/06; Vermont Yankee Nuclear Power Station; Routine
Integrated Report.
This report covered a 13-week period of inspection by resident inspectors and announced inspections by regional engineering and health physics inspectors. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.
NRC-Identified and Self-Revealing Findings
No findings of significance were identified.
B.
Licensee Identified Findings None.
REPORT DETAILS
Summary of Plant Status
Vermont Yankee (VY) Nuclear Power Station began the inspection period operating at 87%
reactor power. At that time, Entergy personnel were performing power ascension testing activities related to an NRC license amendment authorizing an increase in VYs licensed maximum reactor power level from 1593 megawatts thermal (MWth) to 1912 MWth. On April 1, operators increase power to approximately 91%. Power was again increased to approximately 93% and 96% on April 6 and 22, respectively. On April 28, power was increased to 98%.
On May 5, 2006, operators increased reactor power to the new 100% reactor power limit of 1912 MWth.
On May 8, power decreased to approximately 70% during the planned condensate pump trip test performed as part of power ascension testing activities. Following the successful completion of the condensate pump trip test, reactor power was returned to 100% on May 9.
On May 17, operators performed a planned power reduction to approximately 55% to perform individual control rod scram time testing, main steam isolation valve (MSIV) closure testing, turbine valve testing, and rod pattern adjustments. Reactor power was subsequently returned to 100% power on May 21.
On May 24, operators reduced reactor power to approximately 58% in response to indications of a fire in the east switchgear room and ground faults within the electrical system. This event also resulted in the declaration of an Unusual Event in accordance with Entergys approved Emergency Plan. (See Section 4OA3 of this report for more details on Entergys response to this event.) Following this event, operators maintained reactor power at approximately 80%
pending the completion of necessary repairs to plant equipment. Reactor power was returned to 100% on May 27 where it remained throughout the remainder of the inspection period, with the exception of minor power reductions to support control rod pattern adjustments.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
1R01 Adverse Weather Protection
.1 Readiness for Seasonal Susceptibilities
a. Inspection Scope
(one sample)
The inspectors reviewed design features and procedural controls established for the residual heat removal service water (RHRSW) system to minimize the impact of river silting on the RHRSW system and associated cooling loads (i.e., the residual heat removal (RHR) system). River silting is a phenomenon typically associated with springtime snow melt and runoff conditions that result in high flow, high silt conditions on the Connecticut River but can also be a concern throughout the year following periods of heavy rain. The impact of river silt on the RHRSW system is minimized by the silt removal capability of the service water (SW) system strainers (upstream of the RHRSW system) and by maintaining a minimum flow of water through the RHRSW pump motor cooling lines. The inspectors performed walkdowns of the accessible portions of the RHRSW and SW systems and compared the current system alignments and established RHRSW pump cooling flow to the requirements of Vermont Yankee Operating Procedures (OP) 2124, Residual Heat Removal System; OP 2181, Service Water/Alternate Cooling Operating Procedure; OP 0150, Conduct of Operations and Operator Rounds; Technical Specifications (TS); and the Update Final Safety Analysis Report (UFSAR). The inspectors also reviewed condition reports (CRs) to verify that identified silting and other weather-related issues were entered into the corrective action program and appropriate actions were completed or planned to properly resolve the issues.
b. Findings
No findings of significance were identified.
1R04 Equipment Alignment
a. Inspection Scope
(three samples)
The inspectors performed three partial system walkdowns of risk-significant systems to verify system alignment and to identify any discrepancies that could impact system operability. Observed plant conditions were compared to the applicable standby alignment of equipment specified in OP 2124, Residual Heat Removal System; OP 2117, Standby Gas Treatment; and OP 2126, Diesel Generators. The inspectors also observed valve positions, the availability of power supplies, and the general condition of selected components to verify there were no obvious deficiencies.
The inspectors verified the alignment of the following systems:
- The B train of the RHR system while the A train was out of service for planned maintenance;
- The B train of the standby gas treatment system while the A train was out of service for planned maintenance; and
- The B emergency diesel generator (EDG) while the A EDG was out of service for planned maintenance.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
a. Inspection Scope
(nine samples)
The inspectors identified fire areas important to plant risk based on a review of Entergys Vermont Yankee Safe Shutdown Capability Analysis, the Fire Hazards Analysis, and the Individual Plant Examination External Events (IPEEE). The inspectors toured plant areas important to safety in order to verify the suitability of Entergys control of transient combustibles and ignition sources, and the material condition and operational status of fire protection systems, equipment, and barriers. The following fire areas (FAs) and fire zones (FZs) were inspected.
- East Switchgear Room (FA-4);
- West Switchgear Room (FA-5);
- A EDG Room (FA-8);
- B EDG Room (FA-9);
- Cable Vault (FZ-2);
- Battery Room (FZ-3);
- Reactor Building, 280 foot elevation, North (FZ RB5);
- Reactor Building, 280 foot elevation, South (FZ RB6); and
- Relay House - 345 kilovolt (no fire designation).
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures
a. Inspection Scope
(one sample)
The inspectors reviewed Entergys established flood protection barriers and procedures for coping with external flooding events. The inspectors reviewed external flooding information contained in Entergys IPEEE and compared it to required flooding actions delineated in OP 3127, Natural Phenomena. The inspectors performed walkdowns of flood-vulnerable areas and ensured equipment needed to mitigate an external flooding event (e.g., sump pumps, floor drain plugs, sand bags, etc.) was available and in working order. The inspectors also reviewed a sample of problems identified in Entergys corrective action program to verify that Entergy identified and implemented appropriate corrective actions.
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance
a. Inspection Scope
(one sample)
The inspectors performed an annual review to verify the readiness of the A RHR heat exchanger. The inspectors observed Entergys execution of biofouling controls for, and inspections of, the A RHR heat exchanger including the state of cleanliness of the heat exchanger tubes. Following the completion of these activities, the inspectors performed walkdowns of the A RHR heat exchanger to observe inlet and outlet temperatures, primary and secondary side fluid flows, and to look for evidence of leakage.
Observed temperatures and flow rates were compared to expected values contained in OP 2124, Residual Heat Removal System, the TS, and the UFSAR. The inspectors also reviewed a sample of problems identified in Entergys corrective action program to verify that Entergy identified and implemented appropriate corrective actions.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
a. Inspection Scope
(one sample)
The inspectors observed simulator-based licensed operator requalification training provided to operators regarding the expected plant response to a trip of either a feedwater pump or a condensate pump from the new extended power uprate (EPU)100% reactor power level. Training included a discussion of expected plant response(s)and a series of simulator scenarios requiring operators to respond to simulated condensate pump and feedwater pump trips. The inspectors evaluated crew performance in the areas of clarity and formality of communications; ability to take timely actions; prioritization, interpretation, and verification of alarms; procedure use; control board manipulations; oversight and direction from supervisors; and command and control. Crew performance in these areas was compared to Entergy management expectations and guidelines as presented in Vermont Yankee Administrative Procedure (AP) 0151, Responsibilities and Authorities of Operations Department Personnel; AP 0153, Operations Department Communication and Log Maintenance; and Vermont Yankee Department Procedure (DP) 0166, Operations Department Standards.
The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed Entergy evaluators to verify that they also noted the issues to be discussed with the crew.
Additionally, the inspectors observed the fidelity of the plant-specific simulator and compared it to actual plant response(s) and to the requirements of American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.5-1998, Nuclear Power Plant Simulators for Use in Operator Training and Examination.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
(three samples)
The inspectors performed three issue/problem-oriented inspections of actions taken by Entergy in response to the inability of operators to fully open D SW pump discharge valve SW-2D, the failure of the A reactor building-to-torus vacuum breaker to open within in-service testing acceptance criteria during surveillance testing, and the observation of inconsistent closure of an east switchgear room fire damper (FPD-115-12) which is required to close during an actuation of the switchgear room carbon dioxide (CO2) fire suppression system. The inspectors reviewed work practices that may have contributed to degraded system performance, Entergys ability to identify and address common cause failures, the applicable maintenance rule scoping document for each system, the current classification of these systems in accordance 10 CFR 50.65 (a)(1) or (a)(2), and the appropriateness of the performance criteria and goals established for each system.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessment and Emergent Work Evaluation
a. Inspection Scope
(six samples)
The inspectors evaluated online risk management for four planned maintenance activities and two emergent repair activities. The inspectors reviewed maintenance risk evaluations, work schedules, recent corrective actions, and control room logs to verify that other concurrent or emergent maintenance activities did not significantly increase plant risk. The inspectors compared reviewed items and activities to requirements listed in AP 0125, "Plant Equipment" and AP 0172, "Work Schedule Risk Management -
Online." The inspectors reviewed the following work activities:
- Planned maintenance on the A train of the RHR system;
- Planned maintenance on the A EDG;
- Planned replacement of rod position indicating system (RPIS) power supply, PSX-5;
- Planned de-silting of the deep basin which required the safety-related cooling tower cell 2-1 to be taken out of service;
- Emergent repair of the A reactor building-to-torus vacuum breaker; and
- Emergent replacement of reactor protection system (RPS)/primary containment isolation system (PCIS) Agastat relays 5-12C(X) and 5-12D(X).
b. Findings
No findings of significance were identified.
1R14 Personnel Performance During Non-Routine Plant Evolutions
a. Inspection Scope
(three samples)
The inspectors directly observed and assessed control room operator performance during the following non-routine evolutions:
- The second of four planned 5% reactor power increases in support of extended power uprate on April 1, 2006;
- The third of four planned 5% reactor power increases in support of EPU.
This 5% increase was broken into two separate 2.5% reactor power increases, performed on April 6 and April 22. The increase was performed in two increments due to a hold that had been temporarily placed on EPU testing.
(See Section 4OA5.1 of this report for more detail.); and
- The fourth of four planned 5% reactor power increases in support of EPU. This 5% increase was also broken into two separate 2.5% reactor power increases, performed on April 28 and May 5. The increase was performed in two increments due to two holds that had been placed on EPU testing.
(See Section 4OA5.1 of this report for more detail).
The adequacy of personnel performance, procedure compliance, and use of the corrective action process for all non-routine evolutions were evaluated against the requirements and expectations contained in TS and the following station procedures, as applicable:
- AP 0151, Responsibilities and Authorities of Operations Department Personnel;
- AP 0153, Operations Department Communication and Log Maintenance;
- DP 0166, Operations Department Standards;
- Engineering Request Special Test Instruction (ERSTI) 04-VY1-1409, Power Ascension Test Procedure for Extended Power Conditions 1593 to 1912 MWth;
- OP 0105, Reactor Operations; and
- OP 2403, Control Rod Sequence Exchange with the Reactor Online.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
(six samples)
The inspectors reviewed six operability determinations prepared by Entergy.
The inspectors evaluated the operability determinations against the guidance contained in NRC Inspection Manual, Part 9900, Technical Guidance, Operability Determinations and Functionality Assessments for Resolution of Degraded or Nonconforming Conditions Adverse to Quality or Safety, as well as Entergy procedure ENN-OP-104, Operability Determinations. The inspectors verified the adequacy of the following evaluations of degraded or non-conforming conditions:
- While testing the mechanical hydraulic pressure control system per ERSTI 04-VY1-1409 at 1832 MWth, a hold was placed on testing when Entergy identified steam flow data that exceeded established acceptance criteria;
- During the performance of ERSTI 04-VY1-1409, a hold was placed on testing when operators observed control valve position and steam dome-to-turbine steam chest pressure values that were inconsistent with observed steam flow values;
- Inability to fully open D SW pump discharge valve SW-2D;
- RPS/PCIS Agastat relays 5-12C(X) and 5-12D(X) potentially exceeded their environmental qualification lifetime;
- Oil leak on the auto transformer (345-to-115 kilovolt transformer that supplies the startup transformers in the event of a turbine trip); and
- A EDG jacket water cooling pump leakage.
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing
a. Inspection Scope
(five samples)
The inspectors reviewed five post-maintenance testing (PMT) activities on risk-significant systems. The inspectors either directly observed the testing or reviewed completed PMT documentation to verify that the test data met the required acceptance criteria contained in the TS, UFSAR, and inservice testing program. Where testing was directly observed, the inspectors verified that installed test equipment was appropriate and controlled and that the test was performed in accordance with applicable station procedures. The inspectors also verified that the test activities were adequate to ensure system operability and functional capability following maintenance, systems were properly restored following testing, and any discrepancies were appropriately documented in the corrective action program. The inspectors reviewed the following PMT activities:
- Testing in accordance with OP 4124, Residual Heat Removal and RHR Service Water System Surveillance, following planned maintenance on the A train of RHR;
- Testing in accordance with work order (WO) 05-2027, following the replacement of RPIS power supply PSX-5;
- Testing in accordance with WO 05-5204, following emergent troubleshooting of the A reactor building-to-torus vacuum breaker;
- Testing in accordance with ERT 04-526-03-01, C51/C52 Breaker and Capacitor Bank Functional Test, following the installation of the 115 kilovolt switchyard capacitor banks; and
- Testing in accordance with OP 4126, Diesel Generator Surveillance, following planned maintenance on the A EDG.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
(five samples)
The inspectors observed surveillance testing to verify that the test acceptance criteria specified for each test was consistent with TS and UFSAR requirements, the test was performed in accordance with the written procedure, the test data was complete and met procedural requirements, and the system was properly returned to service following testing. The inspectors observed selected pre-job briefs for the test activities.
The inspectors also verified that discrepancies were appropriately documented in the corrective action program. The inspectors verified that the following surveillance testing activities met the above requirements:
- MSIV quarterly closure testing (in-service test) in accordance with OP 4113, Main and Auxiliary Steam System Surveillance, Section A;
- Core spray pump quarterly operability testing (in-service test) in accordance with OP 4123, Core Spray System Surveillance, Section C;
- SW pump operability and discharge check valve quarterly testing (in-service test)in accordance with OP 4181, Service Water/Alternate Cooling System Surveillance, Section A;
- High pressure coolant injection (HPCI) steam line high flow instrument calibration (routine surveillance) in accordance with OP 4356, HPCI Steam Line Flow Functional/Calibration, Section B; and
- Control rod scram time testing (in-service test) in accordance with OP 4424, Control Rod Scram Testing and Data Recording, Section B.
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications
a. Inspection Scope
(one sample)
The inspectors reviewed temporary alteration (TA) 2006-006 made to the circulating water system deicing gate to install restraints to hold the gate closed pending installation of a newly designed deicing gate. The deicing gate can be opened during winter conditions to admit a flow of warm, recirculated circulating water from the discharge structure to the SW intake bay to melt ice buildup. The original gate guide frame and anchorage had degraded and would no longer support the gate in the closed position.
The inspectors compared the information in the TA package to requirements contained in Entergy Nuclear Management Manual Procedure EN-DC-136, Temporary Alterations. The inspectors observed the installation of the TA and verified that required tags were applied and that the alteration was properly maintained.
b. Findings
No findings of significance were identified.
RADIATION SAFETY
Cornerstone: Public Radiation Safety
2PS3 Radiological Environmental Monitoring Program (REMP) (71122.03)
a. Inspection Scope
(one sample, 02.02.e)
During the initial power increase into the EPU range of operation, the inspectors reviewed the effects on offsite dose with respect to 10 CFR 20.1301(e) and 40 CFR 190 public dose limits. The inspectors witnessed pressurized ion chamber data collection at the highest offsite dose location at the VY fence (location DR-53) on March 5, 2006, during the initial EPU power increase, and again on May 5, 2006 once the 100% EPU power level was reached. Entergys basis for accurate dose rate measurement and correlations with main steam line radiation monitors were evaluated. This included reviews of applicable procedure and instrument vendor manuals, as well as calibration records for the pressurized ion chamber and main steam line radiation monitor instrumentation. In addition, the licensees process of data collection, background subtraction, and data reduction was witnessed and reviewed. Inspectors performed an inspection of Entergys REMP program during the fourth quarter of 2005. During this inspection, unresolved item (URI)05000271/2005005-03, Information Needed to Validate the Direct Dose Calculation Method in Offsite Dose Calculation Manual (ODCM) Section 6.11.1, was opened because additional information was required for the inspectors to determine the adequacy of the direct dose calculation methodology in the ODCM. Since then, an in-office review of the licensees technical basis for the direct dose calculation methodology contained in Section 6.11.1 of the ODCM was performed with assistance from the NRCs Office of Nuclear Reactor Regulation (NRR). The purpose of the review was to determine whether the calculation was correct and provided acceptable results to determine dose to the public from VY power operations.
This evaluation was completed on May 16, 2006.
b. Findings
No findings of significance were identified. With the installation of additional turbine shielding on May 17, 2006, the current calculation in Section 6.11.1 of the ODCM is conservative. Entergy plans to conduct another power ascension fence line dose measurement correlation with main steam line radiation monitor measurement at the next outage opportunity and revise Section 6.11.1, accordingly. Inspection and in-office review of this issue has determined that the licensees offsite dose during EPU operation as determined by the calculation method in the ODCM is adequate and that offsite doses are within the NRC and Environmental Protection Agency (EPA) public dose limits. Based on this inspection and in-office review, Unresolved Item 05000271/2005005-03 is closed.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a. Inspection Scope
(two samples)
The inspectors sampled Entergy submittals for the two performance indicators (PIs)listed below for the period from April 2004 to March 2006. PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline; EN-LI-114, Performance Indicator Process; and AP 0094, NRC Performance Indicator Reporting were used to verify the basis in reporting for each data element.
- Reactor Coolant System Specific Activity; and
- Reactor Coolant System Leakage.
The inspectors reviewed portions of operator logs and raw PI data developed from monthly operating reports and discussed the methods for compiling and reporting the PIs with cognizant licensing, operations, and chemistry department personnel.
The inspectors compared graphical representations from the most recent PI report to the raw data to verify that the data was correctly reflected in the report.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Review of Items Entered into the Corrective Action Program
a. Inspection Scope
The inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify they were being entered into Entergys corrective action program at an appropriate threshold and that adequate attention was being given to timely corrective actions. Additionally, in order to identify repetitive equipment failures and/or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into Entergys corrective action program. This review was accomplished by reviewing the description of each new CR and/or by attending daily CR screening meetings. A listing of CRs and other documents reviewed is included in the attachment to this report.
b.
Assessments and Observations No findings of significance were identified.
.2 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of Entergys corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The review was focused on human performance-related issues and considered the results of reviews discussed in Section 4OA2.1. The inspectors review nominally considered the six-month period of January through June 2006. The inspectors compared their results with the results contained in Entergys quarterly trend report for the first quarter 2006; recently developed trend condition reports; Entergys human performance PI data; and discussions with Operations, Radiation Protection (RP), and Technical Support Department management. The corrective actions assigned to address the individual issues as well as to address human performance trends were reviewed for adequacy.
b.
Assessment and Observations No findings of significance were identified.
In May 2006, the Operations Manager initiated trending CR 2006-1492 that summarized two recent Operations Department human performance errors. These errors included operator manipulation of an incorrect valve while attempting to remove the C condensate demineralizer from service and an operator inadvertently tripping open a breaker associated with the EDGs while hanging a tag on an adjacent breaker. As a result of these errors, the Operations Department Human Performance PI turned Red.
Also in May, the RP manager initiated trending CR 2006-1314 summarizing six recent human performance precursor events. For example, an RP technician contaminated himself while performing a survey, there were multiple examples of high radiation area entries without a radiological conditions briefing, and a seavan radioactive material container was missing a required lock.
Operations Department Management held a stand down to brief operating crews on the individual issues listed in CR 2006-1492 and the apparent trend in human performance errors. Additionally, Operations Department Management plans to develop a human performance improvement plan and to perform focused assessments of human performance-related errors and events. Likewise, RP Department Management held a stand down to brief RP personnel on the individual issues and the trend in human performance error precursors and will continue to maintain a heightened level of awareness to human performance-related issues and events.
The inspectors concluded that Operations and RP Department Management made appropriate use of available tools such as the trending process and the PI process to recognize and take action on low level human performance issues before they became more significant and rose to the level of a finding or violation. However, the inspectors also stressed the need for continued diligence in the area of human performance.
.3 Annual Sample Review - Special Nuclear Material Controls
a. Inspection Scope
(one sample)
On April 20, 2004, Entergy determined that two spent fuel rod pieces were not in the storage location designated in the special nuclear material (SNM) inventory records.
On July 13, 2004, following an investigation, Entergy discovered that the two spent fuel rod pieces were still in the spent fuel pool, but in a different location. In 2004, NRC conducted a special inspection to review Entergys investigation and conclusions regarding the search for the two spent fuel rod pieces (Inspection Report 05000271/2004007, dated December 2, 2004). On June 22, 2005, NRC issued a Severity Level III Notice of Violation with no civil penalty to Entergy for failure to keep adequate records of the SNM in its possession and failure to conduct adequate physical inventories (EA 04-0174).
The purpose of this inspection was to review the corrective actions taken by Entergy to address the identified root causes of the failure to account for the spent fuel rod pieces.
The inspectors reviewed the corrective actions completed since September 2004, and assessed the effectiveness of the corrective actions in addressing the identified causes of the event. Specifically, the inspectors reviewed CRs associated with the misplaced spent fuel rod pieces, and other CRs associated with SNM controls initiated since September 2004. The inspectors also reviewed assessments of SNM controls performed by Entergy. The inspector reviewed procedures for control of SNM that had been revised to address the causes of the event, and reviewed records of SNM inventories completed since September 2004. The inspector also toured the refuel floor and held discussions with reactor engineering personnel.
b. Findings and Observations
No findings of significance were identified.
The inspectors found that Entergy had taken significant actions to improve SNM controls since the event in 2004. Procedures were revised and processes were changed to establish detailed controls for transfer and tracking of SNM with an appropriate level of management oversight. There were two instances in which tamper seals for SNM containers were found broken (no material was misplaced) in 2004 and 2005. In both cases, Entergy appropriately considered the effectiveness of previous corrective actions and took further actions to prevent recurrence.
Entergy had performed several assessments of SNM controls since the loss of accountability of the fuel rod pieces in 2004. The inspectors questioned the timing of the licensees effectiveness review of the corrective actions for the event because, at the time it was performed in June 2005, no fuel transfers had been performed and the 2005 annual inventory had not yet been conducted. Although the effectiveness review was not performance based, a Quality Assurance (QA) surveillance was subsequently performed which included observations of SNM transfers during refueling outage (RFO)25 and conduct of the 2005 annual inventory. Entergy also conducted a self-assessment of SNM controls during RFO 25 and the 2005 annual inventory, and a corporate assessment of SNM controls at Vermont Yankee was completed in early 2006.
Based on the results of this inspection, VIO 05000271/2004007-01, Did Not Keep Adequate Records, Follow Procedures, and Perform Physical Inventory of Special Nuclear Material, (EA 04-0174) is closed.
.4 Annual Sample: Failure of Emergency Diesel Generator Loss of Field Relays
a. Inspection Scope
(one sample)
The inspectors reviewed Entergys corrective actions in response to CR 2005-3854, "DG-1-1A and DG-1-1B loss of field relays may not adequately protect the EDGs during a loss of field event when operating in parallel with the grid." The inspectors reviewed CRs, night orders, work orders, plant drawings and engineering documentation as listed in the attachment to this report. The inspectors also performed walkdowns of the EDGs and interviewed operations and engineering department personnel to determine if Entergy had adequately resolved the issues.
b. Findings and Observations
No findings of significance were identified.
Entergys identification of the cause of the B emergency diesel generator failure and the associated corrective actions were appropriate. However, the inspectors identified that an interim administrative control measure was not maintained to ensure that the EDGs were appropriately secured during a loss of field event while paralleled with offsite power or the main generator. An entry was originally made in the Operations Night Orders shortly after identification of the issue (November 2005) that alerted operators to the lack of field-loss protection. This entry reminded operators to monitor field volts and output voltage during surveillance testing, to trip the EDG immediately upon indication of an EDG loss of field, and that the preferred method for tripping the EDG was by using the Test switch in the main control room. The inspectors identified that the entry was removed from the Night Orders on approximately February 16, 2006, without transferal to another administrative process despite the continuing lack of protection.
Modifications to the EDG loss of field relays are scheduled to occur later in 2006.
Entergy entered this issue into their corrective action program (CR 2006-1438) and incorporated the information into the pre-job briefing form used during monthly EDG surveillances. This finding was minor because operators had received licensed operator requalification training on the November 2005 EDG event, which included the associated operator responses, and operating procedures were in place to take appropriate emergency actions in the case of abnormal EDG performance.
4OA3 Event Followup
.1 Indications of a Fire in the East Switchgear Room and the Declaration of an Unusual
Event
a. Inspection Scope
(one sample)
The inspectors responded to the site following the declaration of an Unusual Event (UE)on May 24. The UE was declared on the basis of indications of an in-plant fire that was not extinguished within 10 minutes. The inspectors observed reactor plant parameters in the control room and evaluated safety system response to the event. The inspectors also assessed the response of the licensed operators against applicable operating procedures, abnormal operating procedures, and emergency operating procedures.
The inspectors evaluated Entergys classification of the event as a UE against the Emergency Plan Emergency Action Level (EAL) procedures and the ability of emergency response staff to notify NRC and State/Local Governments as required.
The inspectors also evaluated the response of Entergys fire brigade and the east switchgear room automatic fire protection systems.
b. Findings
The event appears to have been initiated by a ground fault that developed in the windings of the C condensate pump motor. The resultant fault current was transferred, by design, to a resistor bank located in the east switchgear room on bus 2.
This resistor bank is designed to dissipate the current generated during a ground fault in the form of heat. Initial fire brigade reports from the east switchgear room indicated that there were no signs of flames or smoke in the vicinity of the C condensate pump breaker. However, the heat generated by the resistor bank appears to have been sufficient to have ionized dust that had accumulated on and around the resistor bank.
It is believed that the ionized dust caused adjacent fire detectors to alarm and actuate the automatic CO2 fire suppression system. Similar switchgear room CO2 discharge events occurred at VY during motor ground faults in 1983 and 1989. As of the conclusion of this inspection, Entergy had not completed their root cause analysis of this event. Additionally, the inspectors continue to review internal and external operating experience (OE) related to pump motor ground faults, large motor preventive maintenance, and adverse effects of dust accumulation on electrical equipment.
Pending the completion of the inspectors review of Entergys root cause analysis and applicable OE, these issues are considered to be an unresolved item (URI):
URI 0500271/2006003-01, Condensate Pump Motor Fault and Switchgear Room CO2 Initiation Result in the Declaration of an Unusual Event.
4OA5 Other
.1 Power Uprate: Power Ascension Testing
a. Inspection Scope
(four samples)
The inspectors observed power ascension testing performed in accordance with attachments to test procedure ERSTI-04-VY1-1409. The four inspection samples comprised level and pressure testing at 1752, 1832, and 1912 MWth as well as a condensate pump trip test conducted within 7 days of reaching 1912 MWth. The inspectors observed testing to verify that the test acceptance criteria specified was consistent with TS and UFSAR requirements, the test was performed in accordance with the written procedure, test data was complete and met procedural requirements, and affected systems were properly returned to service following testing.
The inspectors also observed selected testing pre-job briefs. The inspectors verified that discrepancies identified during testing were appropriately documented in the corrective action program. The inspectors verified that the following testing activities met the above requirements:
- Testing at 1752 MWth 7B, Feedwater Level Changes 1752 MWth 8B, MHC [mechanical hydraulic control] Pressure Change Demonstration 1752 MWth
- Testing at 1832 MWth 7C, Feedwater Level Changes 1832 MWth 8C, MHC Pressure Change Demonstration 1832 MWth
- Testing at 1912 MWth 7D, Feedwater Level Changes 1912 MWth 8D, MHC Pressure Change Demonstration 1912 MWth
- Condensate Pump Trip Testing 18, Condensate Pump Trip Test at Full EPU Power At 1793 MWth, 1832 MWth, and 1872 MWth, the licensee identified conditions that met Level 2 acceptance criteria established in ERSTI-04-VY1-1409 and required a hold be placed on further testing pending review of the data by Engineering Department personnel and NRC staff, as appropriate. The conditions identified included A main steam line strain gage data that exceeded acceptance criteria at 1793 MWth; steam flow indication variability that exceeded acceptance criteria and operator-observed inconsistencies between indicated steam flow, control valve position, and steam system differential pressure at 1832 MWth; and moisture carryover acceptance criteria was exceeded at 1872 MWth. For each of the holds placed on testing, the inspectors ensured Entergy had entered the issues into their corrective action program and had appropriately evaluated the condition(s) prior to continuing with testing. NRC headquarters staff also reviewed selected issues prior to continuing with testing.
Section 1R15 of this report discusses inspections of the steam flow indication variability and observed inconsistencies between indicated steam flow, control valve position, and steam system differential pressure since these conditions did not specifically require NRC headquarters staff review prior to continuing with testing.
At 1752 MWth and 1912 MWth, the inspectors performed walkdowns of the feedwater heaters, the main condenser and moisture separators, and main steam system piping and valves. The inspectors looked for visual evidence of water and steam leaks and equipment vibration.
b. Findings
No findings of significance were identified.
.2 (Closed) URI 05000271/2006002-01:
Training Provided to Licensed Operators Regarding Plant Response to a Condensate Pump Trip During the observation of training initially provided to licensed operators on the expected plant response to a trip of a condensate pump from 100% reactor power, the inspectors noted that the simulated plant response differed from the predicted plant response indicated in Reactor Engineerings analysis for this event. The difference was in the final values of core thermal power and core flow immediately following the pump trip.
At that time, the inspectors were concerned that the condensate pump trip training initially provided to licensed operators did not meet the met the guidance outlined in American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.5-1998, Nuclear Power Plant Simulators for Use in Operator Training and Examination. Based on the results of the inspections of licensed operator training discussed in Section 1R11 and on the results of the inspections of the condensate pump trip test discussed in Section 4OA5.1, the inspectors concluded that the condensate pump trip training provided to licensed operators met the guidance outlined in ANSI/ANS-3.5-1998.
This URI is closed.
.3 (Closed) NRC Temporary Instruction (TI) 2515/165, Operational Readiness of Offsite
Power and Impact on Plant Risk
a. Inspection Scope
The objective of TI 2515/165, "Operational Readiness of Offsite Power and Impact on Plant Risk," was to gather information to support the assessment of nuclear power plant operational readiness of offsite power systems and impact on plant risk. The inspectors evaluated licensee procedures against the specific offsite power, risk assessment and system grid reliability requirements of TI 2515/165. They also discussed the attributes with licensee personnel.
The information gathered while completing this TI was forwarded to the Office of Nuclear Reactor Regulation for further review and evaluation on April 3, 2006.
b. Findings
No findings of significance were identified.
.4 Institute of Nuclear Power Operations (INPO)/World Association of Nuclear Operators
(WANO) Plant Assessment Report Review The inspectors reviewed the final report for the INPO/WANO plant assessment of the Vermont Yankee Power Station conducted in April 2005. The inspectors reviewed the report to ensure that issues identified were consistent with the NRC perspectives of Entergys performance and to verify if any significant safety issues were identified that required further NRC follow-up.
4OA6 Meetings, Including Exit
Exit Meeting Summary
On July 12, the resident inspectors presented the inspection results to Messrs. Bill Maguire and John Dreyfuss and members of the VY staff. The inspectors asked whether any materials examined during the inspection should be considered proprietary.
No proprietary information was identified.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Entergy Personnel
- J. Devincentis, Licensing Manager
- J. Dreyfuss, Director of Engineering
- M. Hamer, Licensing
- W. Maguire, General Manager of Plant Operations
- K. Pushee, Radiation Protection Manager
- N. Rademacher, Director of Nuclear Safety
- J. Thayer, Site Vice President (former)
- T. Sullivan, Site Vice President (current)
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
- 05000271/2006003-01 URI Condensate Pump Motor Fault and Switchgear Room CO2 Initiation Result in the Declaration of an Unusual Event (Section 4OA3.1)
Closed
- 05000271/2004007-01 VIO Did Not Keep Adequate Records, Follow Procedures, and Perform Physical Inventory of Special Nuclear Material (Section 4OA2.3)
- 05000271/2005005-03 URI Information Needed to Validate the Direct Dose Calculation Method in ODCM Section 6.11.1 (Section 2PS3)
- 05000271/2006002-01 URI Training Provided to Licensed Operators Regarding Plant Response to a Condensate Pump Trip (Section 4OA5.2)