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==SUBJECT:==
==SUBJECT:==
HOPE CREEK GENERATING STATION UNIT 1
HOPE CREEK GENERATING STATION UNIT 1 - INTEGRATED INSPECTION REPORT 05000354/2018004
- INTEGRATED INSPECTION REPORT 05000354/2018004


==Dear Mr. Sena:==
==Dear Mr. Sena:==
On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Hope Creek Generating Station (HCGS). On January 16, 2019 , the NRC inspectors discussed the results of this inspection with Mr. Eric Carr, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report. NRC inspectors documented one finding of very low safety significance (Green) in this report which involved a violation of NRC requirements. Further, inspectors documented a PSEG-identified violation which was determined to be of very low safety significance in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Hope Creek Generating Station (HCGS). On January 16, 2019, the NRC inspectors discussed the results of this inspection with Mr. Eric Carr, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.


If you contest the violations or the significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at HCGS. In addition, if you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at HCGS. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR ) Part 2.390, "Public Inspections, Exemptions, Requests for Withholding."
NRC inspectors documented one finding of very low safety significance (Green) in this report which involved a violation of NRC requirements. Further, inspectors documented a PSEG-identified violation which was determined to be of very low safety significance in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
 
If you contest the violations or the significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
 
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at HCGS. In addition, if you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at HCGS. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR ) Part 2.390, Public Inspections, Exemptions, Requests for Withholding.


Sincerely,
Sincerely,
/RA/ Fred L. Bower , III , Chief Reactor Projects Branch 3 Division of Reactor Projects Docket No.
/RA/  
 
Fred L. Bower, III, Chief Reactor Projects Branch 3 Division of Reactor Projects  
 
Docket No.


50-354 License No.
50-354 License No.
Line 37: Line 44:


===Enclosure:===
===Enclosure:===
Inspection Report 05000 354/20 18004
Inspection Report 05000354/2018004


==Inspection Report==
==Inspection Report==
Docket Number: 50-354 License Number: NPF-57 Report Number: 05000354/2018004 Enterprise Identifier:
Docket Number:
I-2018-004-0010 Licensee: PSEG Nuclear LLC (PSEG)
50-354  
Facility: Hope Creek Generating Station (HCGS)
 
Location: Hancocks Bridge, NJ 08038 Inspection Dates: October 1, 2018 to December 31, 2018 Inspectors:
License Number:
J. Hawkins, Senior Resident Inspector S. Haney, Resident Inspector J. Brand, Senior Reactor Inspector J. DeBoer, Emergency Preparedness Inspector J. Furia, Senior Health Physicist T. Fish, Senior Operations Engineer Approved By:
NPF-57  
Fred L. Bower, III, Chief Reactor Projects Branch 3 Division of Reactor Projects
 
Report Number:
05000354/2018004  
 
Enterprise Identifier: I-2018-004-0010  
 
Licensee:
PSEG Nuclear LLC (PSEG)  
 
Facility:
Hope Creek Generating Station (HCGS)  
 
Location:
Hancocks Bridge, NJ 08038  
 
Inspection Dates:
October 1, 2018 to December 31, 2018  
 
Inspectors:
J. Hawkins, Senior Resident Inspector  
 
S. Haney, Resident Inspector  
 
J. Brand, Senior Reactor Inspector  
 
J. DeBoer, Emergency Preparedness Inspector  
 
J. Furia, Senior Health Physicist  
 
T. Fish, Senior Operations Engineer  
 
Approved By:
Fred L. Bower, III, Chief  


2
Reactor Projects Branch 3
 
Division of Reactor Projects


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring PSEGs performance at
 
Hope Creek Generating Station (HCGS) Unit 1 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below. Licensee-identified non-cited violations (NCVs) are documented in the following Inspection Results sections of the report: 7115


PSEG's performance at Hope Creek Generating Station (HCGS) Unit 1 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRC's program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below.
===List of Findings and Violations===
Inadequate High Pressure Coolant Injection Trip Unit Preventive Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Reactor Safety -
Mitigating Systems


Licensee-identified non-cited violations (NCVs) are documented in the following Inspection Results sections of the report:
Green NCV 05000354/2018004-01 Closed P.2 - Problem Identification and Resolution-Evaluation 71153 A Green self-revealing non-cited violation (NCV) of Technical Specification (TS) 6.8.1.a,
71152. List of Findings and Violations Inadequate High Pressure Coolant Injection Trip Unit Preventive Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Reactor Safety- Mitigating Systems  Green NCV 05000354/2018004
Procedures and Programs, was identified because PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units, which are circuit cards used in various emergency core cooling systems (ECCS) at HCGS. As a result, on September 26, 2018, a failure of the high pressure coolant injection (HPCI) system high water level trip unit occurred resulting in a blown fuse affecting the operability of HPCI and other A channel ECCS (Residual Heat Removal (RHR) and Core Spray). This resulted in PSEG entering a 12 hour shutdown Technical Specification Action Statement (TSAS)  
-01 Closed P.2 - Problem Identification and Resolution- Evaluation 71153 A Green self-revealing non-cited violation (NCV) of Technical Specification (TS) 6.8.1.a, "Procedures and Programs," was identified because PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units, which are circuit cards used in various emergency core cooling systems (ECCS) at HCGS. As a result, on September 26, 2018, a failure of the high pressure coolant injection (HPCI) system high water level trip unit occurred resulting in a blown fuse affecting the operability of HPCI and other 'A' channel ECCS (Residual Heat Removal (R HR) and Core Spray). This resulted in PSEG entering a 12 hour shutdown Technical Specification Action Statement (TSAS) (TS 3.5.1.c.2), an 8 hour non-emergency report (EN#53625) for the HPCI system being inoperable, and a licensee event report (LER) for a condition that could have prevented the fulfillment of a safety function.
(TS 3.5.1.c.2), an 8 hour non-emergency report (EN#53625) for the HPCI system being inoperable, and a licensee event report (LER) for a condition that could have prevented the fulfillment of a safety function.


Additional Tracking Items Type Issue number Title Inspection Results Section Status LER 05000354/2018
===Additional Tracking Items===
-004-00 High Pressure Coolant Injection System Inoperable due to Failed Fuse 71153 Closed
Type Issue number Title Inspection Results Section Status LER 05000354/2018-004-00 High Pressure Coolant Injection System Inoperable due to Failed Fuse 71153 Closed


=PLANT STATUS=
=PLANT STATUS=


===H ope Creek Generating Station (HCGS) began the inspection period at 100 percent rated thermal power (RTP). On December 6, 2018, Hope Creek reduced power to approximately 69 percent rated thermal power to support planned main turbine valve testing, control rod scram time and settle testing, control rod sequence exchange, and plant repairs, and returned to full power on December 8, 2018. There were no other operational power changes of regulatory significance for the remainder of the inspection period.
Hope Creek Generating Station (HCGS) began the inspection period at 100 percent rated thermal power (RTP). On December 6, 2018, Hope Creek reduced power to approximately 69 percent rated thermal power to support planned main turbine valve testing, control rod scram time and settle testing, control rod sequence exchange, and plant repairs, and returned to full power on December 8, 2018. There were no other operational power changes of regulatory significance for the remainder of the inspection period.


==INSPECTION SCOPES==
==INSPECTION SCOPES==
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess PSEG performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
-rm/doc-collections/insp
-manual/inspection
-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, "Light-Water Reactor Inspection Program - Operations Phase.The inspectors performed plant status activities described in IMC 2515 , Appendix D, "Plant Status" and conducted routine reviews using IP
 
===71152, "Problem Identification and Resolution."
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess PSEG performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.


==REACTOR SAFETY==
==REACTOR SAFETY==
==71111.01 - Adverse Weather Protection==
==71111.01 - Adverse Weather Protection==
 
===Seasonal Extreme Weather (1 Sample)===
===Seasonal Extreme Weather===
{{IP sample|IP=IP 71111.01|count=1}}
 
The inspectors evaluated readiness for seasonal extreme weather conditions prior to seasonal cold temperatures the week of November 26, 2018
The inspectors evaluated readiness for seasonal extreme weather conditions prior to seasonal cold temperatures the week of November 26, 2018


==71111.04 - Equipment Alignment==
==71111.04 - Equipment Alignment==
 
===Partial Walkdown (4 Samples)===
===Partial Walkdown===
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
{{IP sample|IP=IP 71111.04|count=4}}
: (1) C Emergency Diesel Generator (EDG) after the rocker arm lube oil tank was found with elevated moisture levels during the week of October 22, 2018
The inspectors evaluated system configuration s during partial walkdowns of the following systems/trains
: (2) A Primary Containment Instrument Gas (PCIG) system compressor after unsuccessful capacity test and troubleshooting the week of October 22, 2018
:
: (3) B and C Station Service Water (SSW) with the A SSW pump out of service for planned maintenance on October 29, 2018
: (1) 'C' Emergency Diesel Generator (EDG) after the rocker arm lube oil tank was found with elevated moisture levels during the week of October 22, 2018
: (2) 'A' Primary Containment Instrument Gas (PCIG) system compressor after unsuccessful capacity test and troubleshooting the week of October 22, 2018
: (3) 'B' and 'C' Station Service Water (SSW) with the 'A' SSW pump out of service for planned maintenance on October 29, 2018
: (4) Reactor protection system (RPS) relay missing sealant extent of condition inspections on December 12, 2018
: (4) Reactor protection system (RPS) relay missing sealant extent of condition inspections on December 12, 2018


==71111.05AQ - Fire Protection Annual/Quarterly==
==71111.05AQ - Fire Protection Annual/Quarterly==
 
===Quarterly Inspection (5 Samples)===
===Quarterly Inspection===
{{IP sample|IP=IP 71111.05AQ|count=5}}
The inspectors evaluated fire protection program implementation in the following selected areas:
The inspectors evaluated fire protection program implementation in the following selected areas:
: (1) 'C' EDG room during the week of October 22, 2018
: (1) C EDG room during the week of October 22, 2018
: (2) 'B' Variable Frequency Drive pump room during the week of October 29, 2018
: (2) B Variable Frequency Drive pump room during the week of October 29, 2018
: (3) Auxiliary building Heating, Ventilation and Air Conditioning (HVAC), inverters and battery rooms during the week of November 1, 2018
: (3) Auxiliary building Heating, Ventilation and Air Conditioning (HVAC), inverters and battery rooms during the week of November 1, 2018
: (4) Auxiliary and service radwaste building cable tray and battery rooms during the week of November 15, 2018
: (4) Auxiliary and service radwaste building cable tray and battery rooms during the week of November 15, 2018
Line 107: Line 136:


==71111.06 - Flood Protection Measures==
==71111.06 - Flood Protection Measures==
 
===Internal Flooding (1 Sample)===
===Internal Flooding===
{{IP sample|IP=IP 71111.06|count=1}}
 
The inspectors evaluated internal flooding mitigation protections in reactor auxiliaries cooling system room on November 8 and 9, 2018.
The inspectors evaluated internal flooding mitigation protections in reactor auxiliaries cooling system room on November 8 and 9, 2018.


==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
===Operator Requalification (1 Sample)===
The inspectors observed and evaluated a crew of licensed operators in the plants simulator during licensed operator annual requalification operating examination that involved a reactor water cleanup pump trip, loss of the 10D410 125 volts direct current bus, high main turbine vibrations, a loss of offsite power and loss of coolant accident, and reactor vessel flooding on November 20, 2018.
===Operator Performance (1 Sample)===
The inspectors observed and evaluated a planned down power to 69 percent rated thermal power to support planned main turbine valve testing, control rod scram time and settle testing, control rod sequence exchange, and plant repairs on December 6, 2018.


===Operator Requalification===
===Operator Requalification Exam Results (Annual) (1 Sample)===
{{IP sample|IP=IP 71111.11|count=1}}
The inspectors reviewed and evaluated requalification examination results (written and operating test) on December 21, 2018.
The inspectors observed and evaluated a crew of licensed operators in the plant's simulator during licensed operator annual requalification operating examination that involved a reactor water cleanup pump trip, loss of the 10D410 125 volts direct current bus, high main turbine vibrations, a loss of offsite power and loss of coolant accident, and reactor vessel flooding on November 20, 2018. Operator Performance (1 Sample)  The inspectors observed and evaluated a planned down power to 69 percent rated thermal power to support planned main turbine valve testing, control rod scram time and settle testing, control rod sequence exchange, and plant repairs on December 6, 2018. Operator Requalification Exam Results (Annual)
===
{{IP sample|IP=IP 71152|count=1}}
The inspector s reviewed and evaluated requalification examination results (written and operating test) on December 21, 2018.


Operator Requalification Program and Operator Performance (Biennial)
===Operator Requalification Program and Operator Performance (Biennial) (1 Sample)===
(1 Sample)===
The inspectors reviewed and evaluated operator performance, evaluator performance, and simulator performance during the requalification examinations completed on December 19, 2018.
The inspectors reviewed and evaluated operator performance, evaluator performance, and simulator performance during the requalification examinations completed on December 19, 2018.


==71111.12 - Maintenance Effectiveness==
==71111.12 - Maintenance Effectiveness==
 
===Routine Maintenance Effectiveness (2 Samples)===
===Routine Maintenance Effectiveness===
{{IP sample|IP=IP 71111.12|count=2}}
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
: (1) High Pressure Coolant Injection (HPCI) trip unit failure on September 26, 2018
: (1) High Pressure Coolant Injection (HPCI) trip unit failure on September 26, 2018
Line 135: Line 159:


==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=4}}


==={{IP sample|IP=IP 71111.13|count=4}}
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
: (1) Unplanned 'A' Electro-Hydraulic Control (EHC) pump replacement on October 15, 2018
: (1) Unplanned A Electro-Hydraulic Control (EHC) pump replacement on October 15, 2018
: (2) Planned open phase group  
: (2) Planned open phase group B alarm and trip testing on November 28, 2018
'B' alarm and trip testing on November 28, 2018
: (3) Planned A Standby Liquid Control (SLC) pump testing on November 29, 2018
: (3) Planned 'A' Standby Liquid Control (SLC) pump testing on November 29, 2018
: (4) Planned single source of offsite power line-up during open phase testing and switchyard expansion from December 7 through 9, 2018
: (4) Planned single source of offsite power line-up during open phase testing and switchyard expansion from December 7 through 9, 2018


==71111.15 - Operability Determinations and Functionality Assessments==
==71111.15 - Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15|count=3}}
{{IP sample|IP=IP 71111.15|count=3}}
The inspectors evaluated the following operability determinations and functionality assessments:
The inspectors evaluated the following operability determinations and functionality assessments:
: (1) 'D' RHR minimum flow check valve chattering while performing the quarterly surveillance test on October 24, 2018
: (1) D RHR minimum flow check valve chattering while performing the quarterly surveillance test on October 24, 2018
: (2) 'B' SSW pump discharge vent valve configuration control on November 12, 2018
: (2) B SSW pump discharge vent valve configuration control on November 12, 2018
: (3) 'B' and 'D' EDG and HPCI transfer/isolation switch testing during the week of December 12, 2018
: (3) B and D EDG and HPCI transfer/isolation switch testing during the week of December 12, 2018


==71111.18 - Plant Modifications==
==71111.18 - Plant Modifications==
{{IP sample|IP=IP 71111.18|count=2}}


(2 Sample s)  The inspectors evaluated the following temporary modification s:
The inspectors evaluated the following temporary modifications:
: (1) Temporary cooling of the 'B' Reactor Recirculation Pump (RRP) seal purge line during the week of October 29, 2018
: (1) Temporary cooling of the B Reactor Recirculation Pump (RRP) seal purge line during the week of October 29, 2018
: (2) Temporary rewiring of safety
: (2) Temporary rewiring of safety-related inverter fans during the week of November 5, 2018
-related inverter fans during the week of November 5, 2018


==71111.19 - Post Maintenance Testing==
==71111.19 - Post Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=4}}
{{IP sample|IP=IP 71111.19|count=4}}
The inspectors evaluated post maintenance testing for the following maintenance/repair activities
 
:
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
: (1) PCIG compressor troubleshooting, relief valve repairs and retest on October 11, 2018
: (1) PCIG compressor troubleshooting, relief valve repairs and retest on October 11, 2018
: (2) Unplanned loss of the reactor manual control system following power supply replacements on October 30, 3018
: (2) Unplanned loss of the reactor manual control system following power supply replacements on October 30, 3018
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==71111.22 - Surveillance Testing==
==71111.22 - Surveillance Testing==
The inspectors evaluated the following surveillance tests:


The inspectors evaluated the following surveillance tests:
===Routine===
Routine===
{{IP sample|IP=IP 71111.22|count=1}}
{{IP sample|IP=IP 71111.13|count=1}}
: (1) HC.OP-IS.BJ-0001, HPCI Main and Booster Set Inservice and 2-year Comprehensive Pump testing on December 4, 2018  
: (1) HC.OP-IS.BJ-0001, HPCI Main and Booster Set Inservice and 2-year Comprehensive Pump testing on December 4, 2018 I nservice (2 Samples)
: (1) Review of HC-18-008 , Relief Valve, Low
-Low Set Channel Functional Test
- Surveilance Test Interval (STI) Evaluation on October 31, 2018
: (2) Review of HC 014, Control Room Emergency Filtration System Functional Test -STI Evaluation on October 31, 2018


===Cornerstone:  Emergency Preparedness===
===Inservice (2 Samples)===
: (1) Review of HC-18-008, Relief Valve, Low-Low Set Channel Functional Test - Surveilance Test Interval (STI) Evaluation on October 31, 2018
: (2) Review of HC-18-014, Control Room Emergency Filtration System Functional Test -STI Evaluation on October 31, 2018


===71114.04 Emergency Action Level and Emergency Plan Changes
===Cornerstone: Emergency Preparedness===
  ===
===71114.04 Emergency Action Level and Emergency Plan Changes===
{{IP sample|IP=IP 71114.04|count=1}}
{{IP sample|IP=IP 71114.04|count=1}}
The inspectors verified that the changes made to the emergency plan were done in accordance with 10 CFR 50.54(q)(3), and any change made to the Emergency Action Levels, Emergency Plan, and its lower
 
-tier implementing procedures, had not resulted in any reduction in effectiveness of the Plan.
The inspectors verified that the changes made to the emergency plan were done in accordance with 10 CFR 50.54(q)(3), and any change made to the Emergency Action Levels, Emergency Plan, and its lower-tier implementing procedures, had not resulted in any reduction in effectiveness of the Plan.


==71114.06 - Drill Evaluation==
==71114.06 - Drill Evaluation==
===Emergency Planning Drill (1 Sample)===
The inspectors evaluated the conduct of a routine PSEG emergency planning drill on December 7,


===Emergency Planning Drill===
==RADIATION SAFETY==
{{IP sample|IP=IP 71114.06|count=1}}
===Cornerstone: Occupational and Public Radiation Safety===
===71124.01 Radiological Hazard Assessment and Exposure Controls===
{{IP sample|IP=IP 71124.01|count=2}}


The inspectors evaluated the conduct of a routine PSEG emergency planning drill on December 7, 2018.
Contamination and Radioactive Material Control


==RADIATION SAFETY==
The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material.
 
High Radiation Area and Very High Radiation Area Controls


===Cornerstone:  Occupational and Public Radiation Safety===
The inspectors reviewed the procedures and controls for High Radiation Areas, Very High Radiation Areas, and radiological transient areas in the plant.


===71124.01 Radiological Hazard Assessment and Exposure Controls
===71124.02 Occupational ALARA Planning and Controls===
===
{{IP sample|IP=IP 71124.02|count=1}}
{{IP sample|IP=IP 71124.01|count=2}}
Contamination and Radioactive Material Control The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material.


High Radiation Area and Very High Radiation Area Controls The inspectors reviewed the procedures and controls for High Radiation Areas, Very High Radiation Areas, and radiological transient areas in the plant.
Radiological Work Planning


===71124.02 Occupational ALARA Planning and Controls
The inspectors selected the following radiological work activities based on exposure significance for review:
  ===
* RWP 8, Refuel Floor Activities
{{IP sample|IP=IP 71124.02|count=1}}
* RWP 10, Maintenance Support Activities
Radiological Work Planning The inspectors selected the following radiological work activities based on exposure significance for review:
* RWP 12, ISI and Snubber Activities
RWP 8, Refuel Floor Activities RWP 10, Maintenance Support Activities RWP 12, ISI and Snubber Activities RWP 14, Drywell Maintenance Activities
* RWP 14, Drywell Maintenance Activities


==OTHER ACTIVITIES
==OTHER ACTIVITIES - BASELINE==
- BASELINE==
===71151 - Performance Indicator Verification===
{{IP sample|IP=IP 71151|count=1}}


===71151 - Performance Indicator Verification (1 sample)  The inspectors verified PSEG's performance indicator submittals for Safety System Functional Failures from January 1, 2018, through December 29, 2018.
The inspectors verified PSEGs performance indicator submittals for Safety System Functional Failures from January 1, 2018, through December 29, 2018.


==71152 - Problem Identification and Resolution==
==71152 - Problem Identification and Resolution==
===1. Semiannual Trend Review (1 Sample)===
The inspectors reviewed PSEGs corrective action program for trends that might be indicative of a more significant safety issue.


===1. Semiannual Trend Review===
===2. Annual Follow-up of Selected Issues (1 Sample)===
{{IP sample|IP=IP 71152|count=1}}
The inspectors reviewed PSEGs implementation of its corrective action program (CAP)related to the following issues:
: (1) NOTF 20791702, HPCI Warm-up line bypass line isolation valve (F100) excessive package leakage during the week of November 26, 2018


The inspectors reviewed PSEG's corrective action program for trends that might be indicative of a more significant safety issue.
===71153 - Follow-up of Events and Notices of Enforcement Discretion


2. Annual Follow
===1. Events===
-up of Selected Issue s (1 Sample)  The inspectors reviewed PSEG's implementation of its corrective action program (CAP) related to the following issues:
===
: (1) NOTF 20791702, HPCI Warm-up line bypass line isolation valve (F100) excessive package leakage during the week of November 26, 2018 71153 - Follow-up of Events and Notices of Enforcement Discretion 1. Events ===
{{IP sample|IP=IP 71153|count=2}}
{{IP sample|IP=IP 71151|count=2}}
 
The inspectors evaluated PSEG's response during the following non
The inspectors evaluated PSEGs response during the following non-routine evolutions and transients:
-routine evolutions and transients:
: (1) Trip of the 5C feedwater heater on December 12, 2018
: (1) Trip of the '5C' feedwater heater on December 12, 2018
: (2) Safety Relief Valve (SRV) main seat leakage causing condensate induced water hammer and noises in the discharge line to the torus identified on December 20, 2018  
: (2) Safety Relief Valve (SRV) main seat leakage causing condensate induced water hammer and noises in the discharge line to the torus identified on December 20, 2018 2. Licensee Event Reports (1 Sample) The inspectors evaluated the following LER, which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx
 
:
===2. Licensee Event Reports (1 Sample)===
: (1) LER 05000354/2018 00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, dated November 20, 2018 (ADAMS Accession:
The inspectors evaluated the following LER, which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
ML18324A614). The circumstances surrounding this LER are documented in the 'Inspection Results' section of this report.
: (1) LER 05000354/2018-004-00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, dated November 20, 2018 (ADAMS Accession: ML18324A614). The circumstances surrounding this LER are documented in the Inspection Results section of this report.


==INSPECTION RESULTS==
==INSPECTION RESULTS==
Licensee Identified Non
Licensee Identified Non-Cited Violation 71152 This violation of very low safety significant was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
-Cited Violation 71152 This violation of very low safety significant was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non
-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.


Violation:
Violation: Hope Creek Generating Station Renewed Facility Operating License No. NPF-57, Condition 2.C.15.b.3 requires, in part, that no disbursements or payments from the  
Hope Creek Generating Station Renewed Facility Operating License No. NPF
[decommissioning] trust shall be made by the trustee until the trustee has first given the NRC 30 days notice of the payment.
-57, Condition 2.C.15.b.3 requires, in part, that no disbursements or payments from the [decommissioning] trust shall be made by the trustee until the trustee has first given the NRC 30 days' notice of the payment.


Contrary to the above, on occasions between 2001 and 2015, disbursements from the Hope Creek Generating Station decommissioning trust were made by the trustee and the trustee had not first given the NRC 30 days' notice of the payment. Specifically, in 2001, 2012, and 2015, PSEG directed the Bank of New York Mellon (the trustee of the decommissioning trust for Hope Creek Generating Station) to disburse payments equaling $240,449.04 for decommissioning cost estimates. However, PSEG failed to notify the NRC of these disbursements until October 19, 2018 (ML18295A023
Contrary to the above, on occasions between 2001 and 2015, disbursements from the Hope Creek Generating Station decommissioning trust were made by the trustee and the trustee had not first given the NRC 30 days notice of the payment. Specifically, in 2001, 2012, and 2015, PSEG directed the Bank of New York Mellon (the trustee of the decommissioning trust for Hope Creek Generating Station) to disburse payments equaling $240,449.04 for decommissioning cost estimates. However, PSEG failed to notify the NRC of these disbursements until October 19, 2018 (ML18295A023).
).


Significance/Severity:
Significance/Severity: This issue is considered within the traditional enforcement process because the failure to inform the NRC prior to disbursing decommissioning funds impacts the ability of the NRC to perform its regulatory oversight function. As noted in Section 2.2.4 of the NRC Enforcement Policy, such violations are dispositioned using traditional enforcement.
This issue is considered within the traditional enforcement process because the failure to inform the NRC prior to disbursing decommissioning funds impacts the ability of the NRC to perform its regulatory oversight function. As noted in Section 2.2.4 of the NRC Enforcement Policy, such violations are dispositioned using traditional enforcement.


The inspectors evaluated the violation in accordance with the NRC Enforcement Policy and determined that it is appropriately characterized at Severity Level IV (SL IV) because it is similar to the SL IV example violation 6.9.d.7, describing a licensee's failure to provide or make a 15-day or 30-day written report or notification that does not impact the regulatory response by the NRC. For this Hope Creek issue, the inspectors determined that the disbursements were made for acceptable decommissioning expenses and would not have necessitated further inquiry or caused the NRC to object to the payments.
The inspectors evaluated the violation in accordance with the NRC Enforcement Policy and determined that it is appropriately characterized at Severity Level IV (SL IV) because it is similar to the SL IV example violation 6.9.d.7, describing a licensees failure to provide or make a 15-day or 30-day written report or notification that does not impact the regulatory response by the NRC. For this Hope Creek issue, the inspectors determined that the disbursements were made for acceptable decommissioning expenses and would not have necessitated further inquiry or caused the NRC to object to the payments.


Corrective Action Reference
Corrective Action Reference: Notification (NOTF) 20808984  
: Notification (NOTF) 20808984 Minor Violation 71152
: (1) Minor Violation:  During the review of NOTFs written for fire protection activities, the inspectors identified multiple pre
-fire plans (PFPs) that were inadequate as well as 29 other PFPs that had been awaiting revision for up to 13 years. The inspectors determined that PSEG not maintaining current, detailed
, and accurate PFPs available to the fire brigade was contrary to the HCGS license condition, the Updated Final Safety Analysis Report, and PSEG's implementing procedures and was a performance deficiency within their ability to foresee and correct and which should have been prevented.


Screening: The inspectors evaluated the issue above in accordance with the guidance in the NRC's Enforcement Policy, IMC 0612, Appendix B, "Issue Screening," and Appendix E, "Examples of Minor Issues," and determined the issue was a minor violation because, although PSEG was not maintaining current, detailed and accurate PFPs, this deficiency did not significantly impact the fire brigade's ability to fight a fire in the affected fire areas.
Minor Violation 71152
: (1) Minor Violation: During the review of NOTFs written for fire protection activities, the inspectors identified multiple pre-fire plans (PFPs) that were inadequate as well as 29 other PFPs that had been awaiting revision for up to 13 years. The inspectors determined that PSEG not maintaining current, detailed, and accurate PFPs available to the fire brigade was contrary to the HCGS license condition, the Updated Final Safety Analysis Report, and PSEGs implementing procedures and was a performance deficiency within their ability to foresee and correct and which should have been prevented.
 
Screening: The inspectors evaluated the issue above in accordance with the guidance in the NRCs Enforcement Policy, IMC 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues, and determined the issue was a minor violation because, although PSEG was not maintaining current, detailed and accurate PFPs, this deficiency did not significantly impact the fire brigades ability to fight a fire in the affected fire areas.


=====Enforcement:=====
=====Enforcement:=====
PSEG has taken actions to restore compliance by documenting additional NOTFs to revise the inaccurate PFPs identified by the inspectors, as well as planning/scheduling the completi o n of all revisions to every PFP by January 2019.
PSEG has taken actions to restore compliance by documenting additional NOTFs to revise the inaccurate PFPs identified by the inspectors, as well as planning/scheduling the completion of all revisions to every PFP by January 2019.


PSEG did not comply with HCGS License Condition 2.C.(7) which requires PSEG to implement and maintain in effect all provisions of the approved fire protection program as described in the UFSAR Section 9.5.1.5.3 and Appendix 9A.III.K for Administrative Controls states, in part, that "Pre-fire plans are written for all safety
PSEG did not comply with HCGS License Condition 2.C.(7) which requires PSEG to implement and maintain in effect all provisions of the approved fire protection program as described in the UFSAR Section 9.5.1.5.3 and Appendix 9A.III.K for Administrative Controls states, in part, that Pre-fire plans are written for all safety-related areas. Fire Protection Program implementing procedure FP-AA-010, Pre-Fire Plans, requires, in part, that pre-fire plans shall be established for all safety-related areas and areas representing a hazard to safety-related equipment. The procedure also requires that the station establish a formal tracking mechanism to ensure that the pre-fire plans are reviewed and updated as necessary. FP-AA-010 also states that the fire protection supervisor/fire marshal is responsible for ensuring the pre-fire plans are current, including the performance of periodic reviews and updates, as necessary. This constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.
-related areas
.Fire Protection Program implementing procedure FP
-AA-010, Pre-Fire Plans, requires, in part, that pre
-fire plans shall be established for all safety
-related areas and areas representing a hazard to safety-related equipment.


The procedure also requires that the station establish a formal tracking mechanism to ensure that the pre
Observations 71152
-fire plans are reviewed and updated as necessary.
: (1) Corrective Action Program (CAP) Evaluations NRC Inspection Reports (IRs) 2017004 and 2016004, Sections 40A2.2, documented the inspectors Semi-Annual Trend reviews of historical CAP evaluations performed each year since 2013. Since 2017, PSEG has implemented the industry initiatives to improve the effectiveness of issue resolution to enhance safety and efficiency within their CAP and the inspectors summarized the CAP data trend below:


FP-AA-010 also states that the fire protection supervisor/fire marshal is responsible for ensuring the pre
Summarized HCGS CAP Information
-fire plans are current, including the performance of periodic reviews and updates, as necessary. This constitutes a minor violation that is not subject to enforcement action in accordance with the NRC's Enforcement Policy.


Observations 71152
2016 (RFO)2017 2018 (RFO)
: (1) Corrective Action Program (CAP) Evaluations NRC Inspection Reports (IRs) 2017004 and 2016004, Sections 40A2.2, documented the inspectors
RCEs  
' Semi-Annual Trend reviews of historical CAP evaluations performed each year since 2013. Since 2017, PSEG has implemented the industry initiatives to improve the effectiveness of issue resolution to enhance safety and efficiency within their CAP and the inspectors summarized the CAP data trend below:
 
Summarized HCGS CAP Information 2016 (RFO) 2017 2018 (RFO) RCEs 1 1 1 ACEs 21 11 10 CCEs 1 6 5 WGEs 66 41 34 Evaluation Totals: 89 59 50 CA Totals: 324* 197 333* Note:
ACEs  
 
CCEs  
 
WGEs  
 
Evaluation Totals:  
 
CA Totals:
324*
197 333*
Note:
* designate RFO was performed during the calendar year.
* designate RFO was performed during the calendar year.


PSEG's total number of CAP evaluations reduced by approximately 50 percent from 2016 to 2017 and remained approximately the same from 2017 to 2018.
PSEGs total number of CAP evaluations reduced by approximately 50 percent from 2016 to 2017 and remained approximately the same from 2017 to 2018. Although the number of evaluations dropped, the inspectors noted the number of corrective actions remained consistent over the last three years (when considering the difference between refueling outage (RFO) years and non-RFO years).
 
Issue Identification, Evaluation and Resolution The inspectors evaluated a number of notifications generated over the course of the past two quarters by departments that provide input to the quarterly trend reports. The inspectors determined that, in most cases, issues were appropriately evaluated by PSEG staff for potential trends and resolved within the scope of the CAP. Examples of this are documented below:
 
1) FLEX Equipment Reliability and Preventive Maintenance In NRC IR 2018002, the Semi-Annual Trend review section documented an increase in FLEX equipment and preventive maintenance issues. PSEG completed a common cause evaluation (70201140) to address the inspectors previous concerns about the potential adverse trend, and over the past two quarters there has been a reduction in identified FLEX issues. The FLEX engine control module (ECM) and heater relay failures were addressed by the site replacing all of these components on the susceptible equipment and conducting failure analyses on the failed components. (See NOTFs 20800028, 20796584, 20799580, 20803195, and Order 70201699)
 
2) Relay Replacements in the Reactor Protection System During an RF21 RPS relay replacement, the inspectors identified that the relay did not have the required fire protection sealant used as a separation barrier inside of the RPS cabinet. PSEG documented the condition in NOTF 20798788 on June 20, 2018, and NOTF 20800461 on July 18, 2018. The inspectors tracked PSEGs completion of the extent of condition regarding other RPS relays which was performed in December 2018, with no additional deficiencies noted.
 
However, the inspectors noted a few instances where PSEG was not timely or did not recognize, until prompted by the inspectors, that potential adverse trends existed. Examples of this are documented below:


Although the number of evaluations dropped, the inspectors noted the number of corrective actions remained consistent over the last three years (when considering the difference between refueling outage (RFO) years and non-RFO years).
1) SRV Main Seat Leakage In NRC IR 2018002, the Semi-Annual Trend review section documented multiple high SRV tailpipe temperatures and conclusions that two of these SRVs, H and K, were exhibiting signs of main seat leakage. Then, in NRC IR 2018003, an annual sample conducted for H SRV and D MSL issues documented that on September 5, 2018. On that date, PSEG also initiated NOTF 20803213 recommending that engineering review the conclusions and corrective actions from a 2014 causal evaluation (ACE 70168360) due to the inspectors questions. Upon further review, the inspectors noted that PSEG had not taken action on NOTF 20803213 because even though there was automatic relief valve seat leakage it had not progressed and begun generating cyclic noises associated with condensate induced water hammer. In 2014, these noises associated with condensate induced water hammer occurred in the torus approximately ~20 times/min. October 1, 2018, the inspectors noted that PSEG initiated NOTF 20806044 for degrading conditions associated with the H SRV main leakage, and then documented the reoccurrence of the condensate induced water hammer in the torus in NOTF 20814836 on December 20, 2018. As of December 31, 2018, PSEG initiated actions to develop an adverse condition monitoring (ACM) plan and operation technical decision making (OTDM) document for the issue. In addition, PSEG initiated NOTF 20816775 when the inspectors determined that the H SRV main seat leak rate data from August to December 2018 was incorrect and did not include peer checks.


Issue Identification, Evaluation and Resolution The inspectors evaluated a number of notifications generated over the course of the past two quarters by departments that provide input to the quarterly trend reports. The inspectors determined that, in most cases, issues were appropriately evaluated by PSEG staff for potential trends and resolved within the scope of the CAP. Example s of this are documented below:  1) FLEX Equipment Reliability and Preventive Maintenance In NRC IR 2018002, the Semi-Annual Trend review section documented an increase in FLEX equipment and preventive maintenance issues. PSEG completed a common cause evaluation (70201140) to address the inspectors' previous concerns about the potential adverse trend, and over the past two quarters there has been a reduction in identified FLEX issues. The FLEX engine control module (ECM) and heater relay failures were addressed by the site replacing all of these components on the susceptible equipment and conducting failure analyses on the failed components.  (See NOTFs 20800028, 20796584, 20799580, 20803195, and Order 70201699)2) Relay Replacements in the Reactor Protection System During an RF21 RPS relay replacement, the inspectors identified that the relay did not have the required fire protection sealant used as a separation barrier inside of the RPS cabinet. PSEG documented the condition in NOTF 20798788 on June 20, 2018, and NOTF 20800461 on July 18, 2018. The inspectors tracked PSEG's completion of the extent of condition regarding other RPS relays which was performed in December 2018, with no additional deficiencies noted.
2) Fire Drills The inspectors noted during their review that in the last 3 years there has only been one fire drill conducted inside the RCA and that there few variations on fire drill locations. The inspectors observed that the purpose of these fire drills per, FP-AA-014, Fire Protection Training Program, is to assess the readiness of the fire brigade and the adequacy of the fire-fighting strategies, procedures and PFPs. PSEG acknowledged and documented in NOTF 20815151 the need to vary the location of fire drills and to revise PFPs in a timely manner.


However, the inspectors noted a few instances where PSEG was not timely or did not recognize, until prompted by the inspectors, that potential adverse trends existed. Examples of this are documented below:
3) Review of Operating Experience (OE) and Vendor Technical Information The inspectors noted an increase in NOTFs written to address gaps in PSEGs use and review of operating experience and untimely updates to vendor technical information.
1) SRV Main Seat Leakage In NRC IR 2018002, the Semi
-Annual Trend review section documented multiple high SRV tailpipe temperatures and conclusions that two of these SRVs, 'H' and 'K', were exhibiting signs of main seat leakage. Then, in NRC IR 2018003, an annual sample conducted for 'H' SRV and 'D' MSL issues documented that on September 5, 2018. On that date, PSEG also initiated NOTF 20803213 recommending that engineering review the conclusions and corrective actions from a 2014 causal evaluation (ACE 70168360) due to the inspector's questions. Upon further review, the inspectors noted that PSEG had not take n action on NOTF 20803213 because even though there was automatic relief valve seat leakage it had not progressed and begun generating cyclic noises associated with condensate induced water hammer. In 2014, these noises associated with condensate induced water hammer occurred in the torus approximately
~20 times/min. October 1, 2018, the inspectors noted that PSEG initiated NOTF 20806044 for degrading conditions associated with the 'H' SRV main leakage, and then documented the reoccurrence of the condensate induced water hammer in the torus in NOTF 20814836 on December 20, 2018. As of December 31, 2018, PSEG initiated actions to develop an adverse condition monitoring (ACM) plan and operation technical decision making (OTDM) document for the issue. In addition, PSEG initiated NOTF 20816775 when the inspectors determined that the 'H' SRV main seat leak rate data from August to December 2018 was incorrect and did not include peer checks.


2) Fire Drills The inspectors noted during their review that in the last 3 years there has only been one fire drill conducted inside the RCA and that there few variation s on fire drill location s. The inspectors observed that the purpose of these fire drills per, FP
(See NOTFs 20802555, 20801537, 20801634, 20800447, 20803032, 20800510, 20802580, 20801654, 20802392, and 702022203.)
-AA-014, Fire Protection Training Program, is to assess the readiness of the fire brigade and the adequacy of the fire-fighting strategies, procedures and PFPs. PSEG acknowledged and documented in NOTF 20815151 the need to vary the location of fire drills and to revise PFPs in a timely manner. 3) Review of Operating Experience (OE) and Vendor Technical Information The inspectors noted an increase in NOTFs written to address gaps in PSEG's use and review of operating experience and untimely updates to vendor technical information.


(See NOTFs 20802555, 20801537, 20801634, 20800447, 20803032, 20800510, 20802580, 20801654, 20802392
The inspectors evaluated all of the issues above in accordance with the guidance in IMC 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues, and determined the issues were of minor significance because the inspectors did not identify any CAQs that were not appropriately corrected or scheduled for correction in a reasonable period of time as a result of the failure to implement the NOTF screening process appropriately.
, and 702022203.)


The inspectors evaluated all of the issues above in accordance with the guidance in IMC 0612, Appendix B, "Issue Screening," and Appendix E, "Examples of Minor Issues," and determined the issues were of minor significance because the inspectors did not identify any CAQs that were not appropriately corrected or scheduled for correction in a reasonable period of time as a result of the failure to implement the NOTF screening process appropriately. Consequently, these issues were not subject to enforcement action in accordance with the NRC's enforcement policy.
Consequently, these issues were not subject to enforcement action in accordance with the NRCs enforcement policy.


Observation 71152 (2.1) The inspectors reviewed PSEG's corrective actions regarding excessive packing leakage from the HPCI warm-up valve (HD
Observation 71152 (2.1)
-F-100) during the last operating cycle. PSEG initiated corrective action notification 20791702 on April 3, 2018, and performed a n Equipment Reliability Evaluation (RE
The inspectors reviewed PSEGs corrective actions regarding excessive packing leakage from the HPCI warm-up valve (HD-F-100) during the last operating cycle. PSEG initiated corrective action notification 20791702 on April 3, 2018, and performed an Equipment Reliability Evaluation (RE-70200144). PSEG determined the two causes were low packing gland stress and severe valve stem pitting corrosion. The inspectors reviewed this valves historical packing leaks, past operability and reportability evaluations, maintenance rule applicability and effects on performance indicators associated with this issue. The inspectors determined that PSEG conducted an appropriate review of the issue, including an adequate extent of condition review and had implemented timely corrective actions to address the causes of the excessive packing leak. The inspectors noted that PSEG had documented packing leaks on this valve on the last four operating cycles going back to 2013. However, the inspectors could not find documentation to show that a corrective action initiated for a June 12, 2013, excessive packing leak under maintenance work order 60111316 to inspect the valve stem for pitting or damage was properly implemented. The inspectors determined this was a missed corrective action opportunity to identify the degraded valve stem for a problem that has since been corrected. The inspectors determined this performance deficiency was minor because the repeated packing leaks did not impact operability of the valve or HPCI system or any other safety related components and did not require an unplanned power reduction or plant shutdown to implement repairs.
-70200144). PSEG determined the two causes were low packing gland stress and severe valve stem pitting corrosion. The inspectors reviewed this valve's historical packing leaks, past operability and reportability evaluations, maintenance rule applicability and effects on performance indicators associated with this issue.


The inspectors determined that PSEG conducted an appropriate review of the issue, including an adequate extent of condition review and had implemented timely corrective actions to address the causes of the excessive packing leak. The inspectors noted that PSEG had documented packing leaks on this valve on the last four operating cycles going back to 2013. However, the inspectors could not find documentation to show that a corrective action initiated for a June 12, 2013, excessive packing leak under maintenance work order 60111316 to inspect the valve stem for pitting or damage was properly implemented. The inspectors determined this was a missed corrective action opportunity to identify the degraded valve stem for a problem that has since been corrected. The inspectors determined this performance deficiency was minor because the repeated packing leaks did not impact operability of the valve or HPCI system or any other safety related components and did not require an unplanned power reduction or plant shutdown to implement repairs.
Trip Unit Inadequate Preventive Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Reactor Safety - Mitigating Systems


Trip Unit Inadequate Preventive Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Reactor Safety
Green NCV 05000354/2018004-01 Closed P.2 - Problem Identification and Resolution  
- Mitigating Systems  Green NCV 05000354/2018004
- Evaluation 71153 (2.1)
-01 Closed P.2 - Problem Identification and Resolution  
A Green self-revealing NCV of TS 6.8.1.a, Procedures and Programs, was identified because PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units, which are circuit cards used in various ECCS at HCGS. As a result, on September 26, 2018, a failure of the HPCI system high water level trip unit occurred resulting in a blown fuse affecting the operability of HPCI and other A channel ECCS (RHR and CS). This resulted in PSEG entering a 12 hour shutdown TSAS (TS 3.5.1.c.2), an 8 hour non-emergency report (EN# 53625) for the HPCI system being inoperable, and an LER for a condition that could have prevented the fulfillment of a safety function.
- Evaluation 71153 (2.1) A Green self
-revealing NCV of TS 6.8.1.a, "Procedures and Programs," was identified because PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units, which are circuit cards used in various ECCS at HCGS. As a result, on September 26, 2018, a failure of the HPCI system high water level trip unit occurred resulting in a blown fuse affecting the operability of HPCI and other 'A' channel ECCS (RHR and CS). This resulted in PSEG entering a 12 hour shutdown TSAS (TS 3.5.1.c.2), an 8 hour non
-emergency report (EN#
53625) for the HPCI system being inoperable, and an LER for a condition that could have prevented the fulfillment of a safety function.


=====Description:=====
=====Description:=====
HGCS utilizes over 200 individual Rosemount trip modules in 42 functional locations throughout the plant, mainly in the reactor protection, reactor recirculation
HGCS utilizes over 200 individual Rosemount trip modules in 42 functional locations throughout the plant, mainly in the reactor protection, reactor recirculation, and ECCS. The HPCI trip logic is performed by these Rosemount trip units as they are arranged in card files containing multiple units which share a common fuse.
, and ECCS. The HPCI trip logic is performed by these Rosemount trip units as they are arranged in card files containing multiple units which share a common fuse.
 
On September 26, 2018, while operating at 100 percent power, PSEG received indications in the main control room that the HPCI system had become inoperable due to a failed fuse in channel A of the system initiating logic. This failed fuse also affected the A channel of the core spray and LPCI sub-systems. PSEGs immediate investigation isolated the fuse failure to a single component, a Rosemount trip unit, associated with the HPCI system high water level trip (level 8). With the fault isolated by PSEGs troubleshooting, operability was restored to the affected A channel ECCS after being in a 12 hour shutdown TS for 6 hours. PSEG restored HPCI system operability by replacing the failed trip unit on September 27, 2018. As a result, PSEG reported this as a condition that could have prevented the fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(D) to the NRC as LERs 05000354/2018-004-00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, on November 20, 2018.


On September 26, 2018, while operating at 100 percent power, PSEG received indications in the main control room that the HPCI system had become inoperable due to a failed fuse in channel 'A' of the system initiating logic. This failed fuse also affected the 'A' channel of the core spray and LPCI sub
On December 11, 2018, PSEG completed a causal evaluation (ERE 70203043) for the failed HPCI trip unit. This evaluation determined that the C25 capacitor in the Rosemount slave trip unit, model 510DU7, failed after being installed in the plant for 32 years (manufactured  
-systems. PSEG's immediate investigation isolated the fuse failure to a single component, a Rosemount trip unit, associated with the HPCI system high water level trip (level 8). With the fault isolated by PSEG's troubleshooting, operability was restored to the affected 'A' channel ECCS after being in a 12 hour shutdown TS for 6 hours. PSEG restored HPCI system operability by replacing the failed trip unit on September 27, 2018. As a result, PSEG reported this as a condition that could have prevented the fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(D) to the NRC as LERs 05000354/2018 00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, on November 20, 2018. On December 11, 2018, PSEG completed a causal evaluation (ERE 70203043) for the failed HPCI trip unit. This evaluation determined that the C25 capacitor in the Rosemount slave trip unit, model 510DU7, failed after being installed in the plant for 32 years (manufactured ~39 years ago). PSEG concluded that even though a Part 21 on these C25 capacitors failin g had been issued in 1999, this failure was random due to the low frequency of occurrence in the industry and at HCGS. PSEG's corrective actions included replacing the failed trip unit and associated fuse, conducting a failure analysis on the failed trip unit, creating actions to implement a trip unit reliability strategy (either to replace all or replace selected trip units) as recommended by the circuit card performance team and plant health committee (PHC).
~39 years ago). PSEG concluded that even though a Part 21 on these C25 capacitors failing had been issued in 1999, this failure was random due to the low frequency of occurrence in the industry and at HCGS. PSEGs corrective actions included replacing the failed trip unit and associated fuse, conducting a failure analysis on the failed trip unit, creating actions to implement a trip unit reliability strategy (either to replace all or replace selected trip units) as recommended by the circuit card performance team and plant health committee (PHC).


The inspectors reviewed PSEG's evaluation and questioned PSEG about the Part 21 issued in 1999. Rosemount had issued the Part 21 (1999 0) for failures of the C25 capacitor on trip units manufactured prior to date code 8630 (week 30 of 1986). The Part 21 recommended further examination to determine if pre
The inspectors reviewed PSEGs evaluation and questioned PSEG about the Part 21 issued in 1999. Rosemount had issued the Part 21 (1999-31-0) for failures of the C25 capacitor on trip units manufactured prior to date code 8630 (week 30 of 1986). The Part 21 recommended further examination to determine if pre-8630 capacitors were installed and whether or not replacement was warranted. The inspectors noted that PSEGs follow-up actions for the Part 21 reviewed under CR990624091 were to inspect and repair the trip units in stock. These actions were put into PSEGs corrective action program under 60012450, 80002672, and 20042758, but were never completed.
-8630 capacitors were installed and whether or not replacement was warranted. The inspectors noted that PSEG's follow
-up actions for the Part 21 reviewed under CR990624091 were to inspect and repair the trip units in stock. These actions were put into PSEG's corrective action program under 60012450, 80002672, and 20042758, but were never completed.


The inspectors then questioned PSEG's review and implementation of the Circuit Card  
The inspectors then questioned PSEGs review and implementation of the Circuit Card - Rosemount Trip Unit preventive centered maintenance (PCM) template. PSEG initially performed a PCM template evaluation for Rosemount trip units in 2009 (Order 70083963) and then due to PCM template revisions, re-reviewed their own maintenance strategy and their justification in 2015 (70157122, 70162269, 70172811) and 2017 (70169938). The PCM template recommended replacement of the 510DU7 and 710DU trip units on an 18 year frequency. Although this maintenance strategy was approved by PSEGs PHC in 2009, PSEG did not approve funding citing the potential large expense and low failure rate of the units over the life of the plant. PSEGs conclusion in 2009, was re-evaluated in 2015 and 2017, with no additional justification for the decision. PSEG did not create preventive maintenance activities for the replacement of selected trip units based on the risk associated with the trip units failure.
- Rosemount Trip Unit preventive centered maintenance (PCM) template. PSEG initially performed a PCM template evaluation for Rosemount trip units in 2009 (Order 70083963) and then due to PCM template revisions, re
-reviewed their own maintenance strategy and their justification in 2015 (70157122, 70162269, 70172811) and 2017 (70169938). The PCM template recommended replacement of the 510DU7 and 710DU trip units on an 18 year frequency. Although this maintenance strategy was approved by PSEG's PHC in 2009, PSEG did not approve funding citing the potential large expense and low failure rate of the units over the life of the plant. PSEG's conclusion in 2009, was re
-evaluated in 2015 and 2017, with no additional justification for the decision. PSEG did not create preventive maintenance activities for the replacement of selected trip units based on the risk associated with the trip unit's failure.


The inspectors reviewed the most recent PCM template revision for Circuit Card  
The inspectors reviewed the most recent PCM template revision for Circuit Card - Rosemount Trip Units from October 2014. This revision was reviewed by PSEG under 2014 NOTF 20664484 and 2017 Order 70169938 which cut, copied, and pasted the 2009 PCM template evaluation under 2009 Order 70083963
- Rosemount Trip Units from October 2014. This revision was reviewed by PSEG under 2014 NOTF 20664484 and 2017 Order 70169938 which 'cut, copied, and pasted' the 2009 PCM template evaluation under 2009 Order 70083963 ('09)which recommends replacement or refurbishment of the model 510DU7 trip units on a 12 year frequency. The PCM template also states that "the maximum replacement frequency for any critical card should be 30 years.And that "the 30 year maximum attempts to limit the vulnerability of the plant to circuit card failures from the long term effects of corrosion, vibration, trace degradation, and all of a circuit card's failure mechanisms."
: (09) which recommends replacement or refurbishment of the model 510DU7 trip units on a 12 year frequency. The PCM template also states that the maximum replacement frequency for any critical card should be 30 years. And that the 30 year maximum attempts to limit the vulnerability of the plant to circuit card failures from the long term effects of corrosion, vibration, trace degradation, and all of a circuit cards failure mechanisms.


Also, the inspectors found that up until February 2018, PCM template implementation evaluations were performed using Section 4.14 of PSEG procedure MA
Also, the inspectors found that up until February 2018, PCM template implementation evaluations were performed using Section 4.14 of PSEG procedure MA-AA-716-210-1001.
-AA-716-210-1001. Section 4.14.9 requires compilation of information necessary to evaluate the PCM template recommendations, including external documents and industry operating experience (OPEX). PSEG's own OPEX search that was conducted as part of their causal evaluation (ERE 70203043) yielded 4 distinct recent events involving the failure of a C25 capacitor on a Rosemount trip unit that resulted in impacts to other safety
-related systems and entry into short duration shutdown TSASs (NMP '16, Perry '13 & '10, Limerick '09). PSEG procedure MA-AA-716-210 (now ER
-AA-210), Preventive Maintenance (PM) Program, Section 4.2.4 PCM Template Process, states that "all PM's that deviate from the PCM template recommendations require a justification documented in the PM Change Process
."  Because of this, the inspectors determined that the justification used by PSEG to not implement a replacement frequency for their Rosemount trip units in 2017, was inadequate because it did not address the revised replacement/refurbishment frequency of 12 years for the Rosemount trip units, the maximum recommended replacement frequency of 30 years for any critical circuit card, or recent industry operating experience involving similar trip unit failures. Corrective Actions:  PSEG's corrective actions included replacing the failed trip unit and associated fuse, conducting a failure analysis on the failed trip unit, and creating actions to implement a trip unit reliability strategy (either to replace all or replace selected trip units) as recommended by the circuit card performance team and plant health committee (PHC).  .
Corrective Action Reference:  20806069.


Performance Assessment
Section 4.14.9 requires compilation of information necessary to evaluate the PCM template recommendations, including external documents and industry operating experience (OPEX).
:  Performance Deficiency:  PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units. This represented a performance deficiency that was reasonably within the licensee's ability to foresee and correct and should have been prevented.


Screening:  The performance deficiency was determined to be more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone, and adversely affected the cornerstone to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, in this case, because PSEG did not adequately justify the replacement frequency for the trip units which resulted in the loss of safety related ECCS equipment, loss of RPS redundancy, and entry into a short duration shutdown TSAS.
PSEGs own OPEX search that was conducted as part of their causal evaluation (ERE 70203043) yielded 4 distinct recent events involving the failure of a C25 capacitor on a Rosemount trip unit that resulted in impacts to other safety-related systems and entry into short duration shutdown TSASs (NMP 16, Perry 13 & 10, Limerick 09). PSEG procedure MA-AA-716-210 (now ER-AA-210), Preventive Maintenance (PM) Program, Section 4.2.4 PCM Template Process, states that all PMs that deviate from the PCM template recommendations require a justification documented in the PM Change Process.


Significance:  The inspectors determined that this finding was of very low safety significance (Green) using NRC IMC 0609, Appendix A, "The Significance Determination Process for Findings At
Because of this, the inspectors determined that the justification used by PSEG to not implement a replacement frequency for their Rosemount trip units in 2017, was inadequate because it did not address the revised replacement/refurbishment frequency of 12 years for the Rosemount trip units, the maximum recommended replacement frequency of 30 years for any critical circuit card, or recent industry operating experience involving similar trip unit failures.
-Power," Exhibit 2
- Mitigating Systems Screening Questions, dated July 1, 2012, because the finding did not represent a loss of system and/or function, did not represent an actual loss of function of at least a single train for greater than its TS allowed outage time or an actual loss of function of one or more non
-TS trains of equipment designated as high safety-significant in accordance with PSEG's maintenance rule program for greater than 24 hours.


Cross-Cutting Aspect: This finding is related to the cross
Corrective Actions: PSEGs corrective actions included replacing the failed trip unit and associated fuse, conducting a failure analysis on the failed trip unit, and creating actions to implement a trip unit reliability strategy (either to replace all or replace selected trip units) as recommended by the circuit card performance team and plant health committee (PHC)..  
-cutting area of Problem Identification and Resolution, Evaluation, because PSEG did not thoroughly evaluates issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, the inspectors determined that PSEG did not thoroughly re-evaluate the PM replacement justification for safety
-related Rosemount trip units in 2017. (P.2) Enforcement
:    Violation:  TS 6.8.1.a, "Procedures and Programs," requires in part, that written procedures recommended in Appendix A of Regulatory Guide (RG) 1.33, Revision 2, shall be established, implemented, and maintained. Section 9 of RG 1.33, Revision 2, Appendix A, recommends procedures for performing maintenance, including: a. maintenance that can affect the performance of safety
-related equipment should be properly pre
-planned and performed in accordance with written procedures and documented instructions appropriate to the circumstances; and, b. preventive maintenance schedules should be developed to specify the inspection or replacement of parts that have a specific lifetime. In 2017, PSEG's procedure MA
-AA-716-210-1001 for PCM template implementation evaluations details the implementation evaluation process which formally documents and justifies PSEG's approved maintenance strategies.


Contrary to the above, between 2009 and 2017, PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the for Rosemount trip units, which are circuit cards used in various ECCS at HCGS. As a result, on September 26, 2018, a failure of the HPCI system trip unit occurred resulting in a blown fuse affecting the operability of both HPCI and 'A' channel ECCS. This resulted in PSEG entering a 12 hour shutdown Technical Specification, an 8 hour non
Corrective Action Reference: 20806069.
-emergency report for the HPCI system being inoperable, and an LER for a condition that could have prevented the fulfillment of a safety function. PSEG's corrective actions included replacing the failed trip unit and associated fuse and creating actions to implement a trip unit reliability strategy.


Disposition: This violation is being treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.
=====Performance Assessment:=====
Performance Deficiency: PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units. This represented a performance deficiency that was reasonably within the licensees ability to foresee and correct and should have been prevented.
 
Screening: The performance deficiency was determined to be more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone, and adversely affected the cornerstone to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, in this case, because PSEG did not adequately justify the replacement frequency for the trip units which resulted in the loss of safety related ECCS equipment, loss of RPS redundancy, and entry into a short duration shutdown TSAS.
 
Significance: The inspectors determined that this finding was of very low safety significance (Green) using NRC IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2 - Mitigating Systems Screening Questions, dated July 1, 2012, because the finding did not represent a loss of system and/or function, did not represent an actual loss of function of at least a single train for greater than its TS allowed outage time or an actual loss of function of one or more non-TS trains of equipment designated as high safety-significant in accordance with PSEGs maintenance rule program for greater than 24 hours.
 
Cross-Cutting Aspect: This finding is related to the cross-cutting area of Problem Identification and Resolution, Evaluation, because PSEG did not thoroughly evaluates issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, the inspectors determined that PSEG did not thoroughly re-evaluate the PM replacement justification for safety-related Rosemount trip units in 2017.
 
(P.2)
 
=====Enforcement:=====
Violation: TS 6.8.1.a, Procedures and Programs, requires in part, that written procedures recommended in Appendix A of Regulatory Guide (RG) 1.33, Revision 2, shall be established, implemented, and maintained. Section 9 of RG 1.33, Revision 2, Appendix A, recommends procedures for performing maintenance, including: a. maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures and documented instructions appropriate to the circumstances; and, b. preventive maintenance schedules should be developed to specify the inspection or replacement of parts that have a specific lifetime. In 2017, PSEGs procedure MA-AA-716-210-1001 for PCM template implementation evaluations details the implementation evaluation process which formally documents and justifies PSEGs approved maintenance strategies.
 
Contrary to the above, between 2009 and 2017, PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the for Rosemount trip units, which are circuit cards used in various ECCS at HCGS. As a result, on September 26, 2018, a failure of the HPCI system trip unit occurred resulting in a blown fuse affecting the operability of both HPCI and A channel ECCS. This resulted in PSEG entering a 12 hour shutdown Technical Specification, an 8 hour non-emergency report for the HPCI system being inoperable, and an LER for a condition that could have prevented the fulfillment of a safety function. PSEGs corrective actions included replacing the failed trip unit and associated fuse and creating actions to implement a trip unit reliability strategy.
 
Disposition: This violation is being treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.


==EXIT MEETINGS AND DEBRIEFS==
==EXIT MEETINGS AND DEBRIEFS==
The inspectors verified no proprietary information was retained or documented in this report.
The inspectors verified no proprietary information was retained or documented in this report.
* On November 29, 2018 the inspector presented the inspection results of PSEGs implementation of its corrective action program related to the HPCI warmup valve excessive to Tanya Timberman, Regulatory Compliance. The inspectors verified no propertiety information was retained or documented in this report.
* On November 30, 2018, the inspector presented the radiation safety inspection results to H. Trimble, Radiation Protection Manager, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.
* On January 16, 2019, the inspectors presented the quarterly resident inspector inspection results to Mr. Eric Carr, Site Vice President, and other members of the PSEG staff.


On November 29, 2018 the inspector presented the inspection results of PSEG's implementation of its corrective action program related to the HPCI warmup valve excessive to Tanya Timberman, Regulatory Compliance. The inspectors verified no propertiety information was retained or documented in this report.
THIRD PARTY REVIEWS


On November 30, 2018, the inspector presented the radiation safety inspection results to H. Trimble, Radiation Protection Manager, and other members of the licensee staff.
The inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the inspection period.


The inspectors verified no proprietary information was retained or documented in this report.
Observation 71153 (2.1)
Licensee Event Report 05000354/2018-004-00: High Pressure Coolant Injection System Inoperable due to Failed Fuse


On January 16, 2019, the inspectors presented the quarterly resident inspector inspection results to Mr. Eric Carr, Site Vice President, and other members of the PSEG staff. THIRD PARTY REVIEWS The inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the inspection period.
On September 26, 2018, while operating at 100 percent power, PSEG received indications in the main control room that the HPCI system had become inoperable due to a failed fuse in channel A of the system initiating logic. This failed fuse also affected the A channel of the core spray and LPCI sub-systems. PSEGs investigation isolated the fuse failure to a single component, a Rosemount trip unit, associated with the HPCI system high water level trip (level 8). With the fault isolated, operability was restored to the affected A channel emergency core cooling systems. PSEG restored HPCI system operability by replacing the failed trip unit on September 27, 2018. As a result, PSEG reported this to the NRC as a condition that could have prevented the fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(D) as LER 05000354/2018-004-00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, on November 20, 2018. The inspectors performed inspections documented in the Maintenance Effectiveness (71111.12) and Performance Indicator Verification (71151) Sections of this report. The inspectors identified a performance deficiency during the review of this LER and related inspections of the Rosemount trip unit that is documented below. This review closes LER 05000354/2018-004-00.
 
Observation 71153 (2.1) Licensee Event Report 05000354/2018 00:  High Pressure Coolant Injection System Inoperable due to Failed Fuse On September 26, 2018, while operating at 100 percent power, PSEG received indications in the main control room that the HPCI system had become inoperable due to a failed fuse in channel 'A' of the system initiating logic. This failed fuse also affected the 'A' channel of the core spray and LPCI sub
-systems. PSEG's investigation isolated the fuse failure to a single component, a Rosemount trip unit, associated with the HPCI system high water level trip (level 8). With the fault isolated, operability was restored to the affected 'A' channel emergency core cooling systems. PSEG restored HPCI system operability by replacing the failed trip unit on September 27, 2018. As a result, PSEG reported this to the NRC as a condition that could have prevented the fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(D) as LER 05000354/2018 00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, on November 20, 2018. The inspectors performed inspections documented in the Maintenance Effectiveness (71111.12) and Performance Indicator Verification (71151) Sections of this report. The inspectors identified a performance deficiency during the review of this LER and related inspections of the Rosemount trip unit that is documented below. This review closes LER 05000354/2018 00.


=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


Section 1R01:
Section 1R01: Adverse Weather Protection
Adverse Weather Protection
Procedures
Procedures
HC.OP-AB.MISC-0001, Acts of Nature, Revision 33
HC.OP-AB.MISC-0001, Acts of Nature, Revision 33
HC.OP-GP.ZZ-0003, Station Preparations for Winter Conditions, Revision 31
HC.OP-GP.ZZ-0003, Station Preparations for Winter Conditions, Revision 31
Notifications
Notifications
20810731 20811656 20811719 20811837 20811932 20811933 20811934 20813248 Section 1R04:
20810731
Equipment Alignment
20811656
20811719
20811837
20811932
20811933
20811934
20813248
Section 1R04: Equipment Alignment
Procedures
Procedures
HC.OP-FT.KL-0001, Primary Containment Instrument Gas System Comprehensive Capacity Test, Revision
HC.OP-FT.KL-0001, Primary Containment Instrument Gas System Comprehensive Capacity
HC.OP-ST.KJ-0003, Emergency Diesel Generator 1CG400 Operability Test, Revision 7
Test, Revision 1
Notification
HC.OP-ST.KJ-0003, Emergency Diesel Generator 1CG400 Operability Test, Revision 77
s 20798788 20802492 20803055 20803058 20812962* Maintenance Orders/Work Orders
Notifications
60139934 60140087 70202651  Section 1R05: Fire Protection
20798788
20802492
20803055
20803058
20812962*
Maintenance Orders/Work Orders
60139934
60140087
202651
Section 1R05: Fire Protection
Procedures
Procedures
AD-AA-101-1005, Procedure Revision Priority Coding and Expectations, Revision 1
AD-AA-101-1005, Procedure Revision Priority Coding and Expectations, Revision 1
FP-AA-010, Pre-Fire Plans, Revision
FP-AA-010, Pre-Fire Plans, Revision 1
FRH-II-531, HC PFP Diesel Generator Rooms, Revision 8
FRH-II-531, HC PFP Diesel Generator Rooms, Revision 8
FRH-II-541, Class 1E Switchgear Rooms 130' Elevation, Revision
FRH-II-541, Class 1E Switchgear Rooms 130 Elevation, Revision 7
FRH-II-562, HC PFP HVAC Equipment, Inverters and Batteries 163' Elevation, Revision 5
FRH-II-562, HC PFP HVAC Equipment, Inverters and Batteries 163 Elevation, Revision 5
FRH-III-151, HC PFP Turbine Building 137' Elevation, Revision 4
FRH-III-151, HC PFP Turbine Building 137 Elevation, Revision 4
FRH-III-321, Cable Tray Area and Battery Rooms 87' Elevation, Revision 5
FRH-III-321, Cable Tray Area and Battery Rooms 87 Elevation, Revision 5
Notifications
Notifications (*initiated in response to inspection)
(*initiated in response to inspection
20810330*
) 20810330* 20810592* 20810740* 20424016 20629300 20803887 20812821 20814931 20816586 Maintenance Orders/Work Orders
20810592*
60141360 70153147 70204994 80122358 Miscellaneous
20810740*
20424016
20629300
20803887
20812821
20814931
20816586
Maintenance Orders/Work Orders
60141360
70153147
204994
80122358
Miscellaneous
Hope Creek Fire Protection Completed Fire Drill List from 2016 through 2018
Hope Creek Fire Protection Completed Fire Drill List from 2016 through 2018
Hope Creek Fire Protection Night Order / Shift Communication dated October 31, 2018
Hope Creek Fire Protection Night Order / Shift Communication dated October 31, 2018
Hope Creek Fire Protection List of Outstanding Pre
Hope Creek Fire Protection List of Outstanding Pre-Fire Plan Revisions dated
-Fire Plan Revisions dated
November 15, 2018  
November 15, 2018


Section 1R0
Section 1R06: Flood Protection Measures
6: Flood Protection Measures
Procedures
Procedures
HC.OP-ST.EA-0002, Service Water System Functional Test  
HC.OP-ST.EA-0002, Service Water System Functional Test - 18 Months, Revision 5
- 18 Months, Revision 5
Maintenance Orders/Work Orders
Maintenance Orders/Work Orders
50185261 50189406 50190174 Miscellaneous
50185261
HC-PRA-012, Hope Creek Generating Station Probabilistic Risk Assessment Internal Flood Notebook, Revision 3
50189406
Section 1R11:
50190174
Licensed Operator Requalification Program
Miscellaneous
HC-PRA-012, Hope Creek Generating Station Probabilistic Risk Assessment Internal Flood
Notebook, Revision 3
Section 1R11: Licensed Operator Requalification Program
Miscellaneous
Miscellaneous
ESG-015, RWCU Pump Trip, Loss of 10D410, Turbine Vibrations, LOP/LOCA, Rx Flooding, dated November 7, 2018
ESG-015, RWCU Pump Trip, Loss of 10D410, Turbine Vibrations, LOP/LOCA, Rx Flooding,
Section 1R12:
dated November 7, 2018
Maintenance Effectiveness
Section 1R12: Maintenance Effectiveness
Procedures
Procedures
ER-AA-210, Preventive Maintenance (PM) Program, Revision 0
ER-AA-210, Preventive Maintenance (PM) Program, Revision 0
ER-AA-310-1002, Maintenance Rule  
ER-AA-310-1002, Maintenance Rule - SSC Risk Significance Determination, Revision 7
- SSC Risk Significance Determination, Revision 7
ER-AA-600-1015, FPIE PRA Model Update, Revision 8
ER-AA-600-1015, FPIE PRA Model Update, Revision 8
ER-AA-600-1044, Maintenance Rule Support, Revision 5
ER-AA-600-1044, Maintenance Rule Support, Revision 5
HC-MRULE-001, HCGS Probabalistic Risk Assessment  
HC-MRULE-001, HCGS Probabalistic Risk Assessment - HC Maintenance Rule Risk
- HC Maintenance Rule Risk Significance Catergorization, Revision 3
Significance Catergorization, Revision 3
LS-AA-115, Operating Experience Program, Revision 16
LS-AA-115, Operating Experience Program, Revision 16
MA-AA-716-210-1001, Performance Centered Maintenance (PCM Templates), Revision 13
MA-AA-716-210-1001, Performance Centered Maintenance (PCM Templates), Revision 13
Notifications
Notifications
20808273 20808338 20809870 20810854 Maintenance Orders/Work Orders
20808273
60140456 70083963 70157122 70162269 70172811 70203043 70204092  Miscellaneous
20808338
HC Troubleshooting Plan 18
20809870
-168 MTG-2018-00212 Section 1R13:
20810854
Maintenance Risk Assessments
Maintenance Orders/Work Orders
and Emergent Work Control
60140456
70083963
70157122
70162269
70172811
203043
204092
Miscellaneous
HC Troubleshooting Plan 18-168
MTG-2018-00212
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Procedures
Procedures
HC.OP-FT.KJ-0003, Emergency Diesel Generator 1CG400  
HC.OP-FT.KJ-0003, Emergency Diesel Generator 1CG400 - Functional Test, Revision 9
- Functional Test, Revision 9
HC.OP-IS.BH-0003, Standby Liquid Control Pump AP208 - Inservice Test, Revision 16
HC.OP-IS.BH-0003, Standby Liquid Control Pump AP208  
- Inservice Test, Revision 16
OP-HC-108-115-1001, Operability Assessment and Equipment Control Program, Revision 36
OP-HC-108-115-1001, Operability Assessment and Equipment Control Program, Revision 36
WC-AA-101, On-line Work Management Process, Revision 25
WC-AA-101, On-line Work Management Process, Revision 25  


Notifications
Notifications (*initiated in response to inspection)
(*initiated in response to inspection
20807472*
) 20807472* 20777837 20779618 20784239 20794566 20794567 20794715 20798272 20798273 20800410 20807066 208070 78 20807499 20807625 Maintenance Orders/Work Orders
20777837
30322641 60139612 60139613 70197036 Miscellaneous
20779618
Hope Creek Generating Station On
20784239
-Line Risk Assessment, Work Week 842, Applicable Period 10/14/18 - 10/20/18, Revision 0
20794566
Hope Creek Generating Station
20794567
On-Line Risk Assessment, Work Week 842, Applicable Period 10/14/18 - 10/20/18, Revision 1
20794715
Section 1R15:
20798272
Operability Determinations and Functionality Assessments
20798273
20800410
20807066
20807078
20807499
20807625
Maintenance Orders/Work Orders
30322641
60139612
60139613
70197036
Miscellaneous
Hope Creek Generating Station On-Line Risk Assessment, Work Week 842, Applicable Period
10/14/18 - 10/20/18, Revision 0
Hope Creek Generating Station On-Line Risk Assessment, Work Week 842, Applicable Period
10/14/18 - 10/20/18, Revision 1
Section 1R15: Operability Determinations and Functionality Assessments
Procedures
Procedures
HC.IC-CC.BB-0062, Nuclear Boiler  
HC.IC-CC.BB-0062, Nuclear Boiler - Division 4 Channel B21-N707D Safety Relief Valve
- Division 4 Channel B2
B21-F013P Low-Low Set, Revision 9
1-N 707D Safety Relief Valve
HC.IC-FT.BB-0073, Channel A - CS, HPCI, RHR, PCIS Rosemount Trip Units, Revision 6
B 21-F013P Low-Low Set, Revision 9
HC.OP-IS.BC-0104, Residual Heat Removal Subsystem D Valves - Inservice Test, Revision 28
HC.IC-FT.BB-0073, Channel A  
HC.OP-IS.BF-0101, Control Rod System Valves - Inservice Test, Revision 21
- CS, HPCI, RHR, PCIS Rosemount Trip Units, Revision 6
HC.OP-IS.BC-0104, Residual Heat Removal Subsystem D Valves  
- Inservice Test, Revision 28
HC.OP-IS.BF-0101, Control Rod System Valves  
- Inservice Test, Revision 21
OP-AA-108-101-1002, Component Configuration Control, Revision 11
OP-AA-108-101-1002, Component Configuration Control, Revision 11
Notifications
Notifications
20734665 20756667 20772331 20800262 20801704 20806153 20808531 20811707 Maintenance Orders/Work Orders
20734665
229368 5 0183099 50194371 50197720 50199947 50202024 50204029 50204150 50204881 50205499 50205829 50206068 60138614 60139795 70195608 Section 1R18:
20756667
Plant Modifications
20772331
20800262
20801704
20806153
20808531
20811707
Maintenance Orders/Work Orders
229368
50183099
50194371
50197720
50199947
202024
204029
204150
204881
205499
205829
206068
60138614
60139795
70195608
Section 1R18: Plant Modifications
Procedures
Procedures
HC.OP-AB.RPV-0003, Recirculation System/Power Oscillations, Revision 32
HC.OP-AB.RPV-0003, Recirculation System/Power Oscillations, Revision 32
Notifications
Notifications
20793755 20795331 20795496 20796552 20801395 Maintenance Orders/Work Orders
20793755
80122350 80122499 Miscellaneous
20795331
20795496
20796552
20801395
Maintenance Orders/Work Orders
80122350
80122499
Miscellaneous
TCCP 4HT-13-008, Temporary Cooling for the Recirculation Pump Seal Purge Line
TCCP 4HT-13-008, Temporary Cooling for the Recirculation Pump Seal Purge Line
TCCP 4HT-18-012, Temporary Cooling for the Recirculation Pump Seal Purge Line
TCCP 4HT-18-012, Temporary Cooling for the Recirculation Pump Seal Purge Line  


Section 1R19:
Section 1R19: Post-Maintenance Testing
Post-Maintenance Testing
Procedures
Procedures
HC.OP-FT.KL-0001, Primary Containment Instrument Gas System Compressor Capacity Test, Revision 1
HC.OP-FT.KL-0001, Primary Containment Instrument Gas System Compressor Capacity Test,
Revision 1
Notifications
Notifications
20769194 20802492 20808273 20808338 20816502 20816638 Maintenance Orders/Work Orders
20769194
266260 60135779 60135861 60140047 60140456 60141422 80124125 Section 1R22:
20802492
Surveillance
20808273
Testing  Procedures
20808338
ER-AA-450, Implementation of the Technical Specification Surveillance Frequency Control Program, Revision 2
20816502
HC.OP-IS.BJ-0002, HPCI Jockey Pump  
20816638
- AP228 - Inservice Test, Revision 35
Maintenance Orders/Work Orders
266260
60135779
60135861
60140047
60140456
60141422
80124125
Section 1R22: Surveillance Testing
Procedures
ER-AA-450, Implementation of the Technical Specification Surveillance Frequency Control
Program, Revision 2
HC.OP-IS.BJ-0002, HPCI Jockey Pump - AP228 - Inservice Test, Revision 35
LS-AA-106-101, Station Review Committee, Revision 0
LS-AA-106-101, Station Review Committee, Revision 0
Notifications
Notifications
20743957 20803682 Maintenance Orders/Work Orders
20743957
30326348 50192426 50194073 50206595  Miscellaneous
20803682
HC-14-014, Control Room Emergency Filtration System Functional Test STI Evaluation, Revision 0
Maintenance Orders/Work Orders
HC-18-008, Relief Valve, Low
30326348
-Low Set Channel Functional Test Surveillance Test Interval (STI) Evaluation, Revision 0
50192426
HC-STI-022, Risk Evaluation of Surveillance Interval Extension for Low
50194073
-Low Set SRV Operability Test, Revision 0
206595
HC-STI-027, Risk Evaluation of Control Room Emergency Filtration System Functional Test, Revision 0
Miscellaneous
Hope Creek Lubricating Oil Report for H1FD
HC-14-014, Control Room Emergency Filtration System Functional Test STI Evaluation,
-10-S-211 dated October 10, 2018
Revision 0
Section 1EP4: Emergency Action Level and Emergency Plan Changes
HC-18-008, Relief Valve, Low-Low Set Channel Functional Test Surveillance Test Interval (STI)
Evaluation, Revision 0
HC-STI-022, Risk Evaluation of Surveillance Interval Extension for Low-Low Set SRV
Operability Test, Revision 0
HC-STI-027, Risk Evaluation of Control Room Emergency Filtration System Functional Test,
Revision 0
Hope Creek Lubricating Oil Report for H1FD-10-S-211 dated October 10, 2018
Section 1EP4: Emergency Action Level and Emergency Plan Changes
Miscellaneous
Miscellaneous
2018-02, OP-AA-101-111, Roles and Responsibilities of On Shift Personnel, Revision 10
2018-02, OP-AA-101-111, Roles and Responsibilities of On Shift Personnel, Revision 10
2018-21, 80111425  
2018-21, 80111425 - 2R19A-D Steam Generator Blowdown Radiation Monitors
- 2R19A-D Steam Generator Blowdown Radiation Monitors
2018-24, NC.EP-EP.ZZ-0309 Dose Assessment (MIDAS) Instructions Revision 16
2018-24, NC.EP-EP.ZZ-0309 Dose Assessment (MIDAS) Instructions Revision 16
2018-56, Emergency News Center as Backup Emergency Operations Facility
2018-56, Emergency News Center as Backup Emergency Operations Facility
Section 1EP6: Drill Evaluation
Section 1EP6: Drill Evaluation
Procedures
Procedures
EP-AA-125-1002, NRC Drill and Exercise Performance (DEP) Indicator Guidance, Revision 5
EP-AA-125-1002, NRC Drill and Exercise Performance (DEP) Indicator Guidance, Revision 5
EP-HC-111-131, Hope Creek Wall Chart (Hot), Revision 1
EP-HC-111-131, Hope Creek Wall Chart (Hot), Revision 1  


Section 4OA1: Performance Indicator Verification
Section 4OA1: Performance Indicator Verification
Procedures
Procedures
LS-AA-2001 , Collecting and Reporting of NRC Performance Indicator Data, Revision 11
LS-AA-2001, Collecting and Reporting of NRC Performance Indicator Data, Revision 11
LS-AA-2080 , Monthly Data Elements for NRC Safety System Functional Failures, Revision 5
LS-AA-2080, Monthly Data Elements for NRC Safety System Functional Failures, Revision 5
Notifications
Notifications
20791702 20793327 20795822 20799118 20804677 Miscellaneous
20791702
Licensee Event Report 2018
20793327
-004-00, HPCI System Inoperable due to Failed Fuse dated November 20, 2018
20795822
Section 4OA2: Problem Identification and Resolution
20799118
20804677
Miscellaneous
Licensee Event Report 2018-004-00, HPCI System Inoperable due to Failed Fuse dated
November 20, 2018
Section 4OA2: Problem Identification and Resolution
Procedures
Procedures
AD-AA-101-1005, Procedure Revision Priority Coding and Expectations, Revision 1
AD-AA-101-1005, Procedure Revision Priority Coding and Expectations, Revision 1
FP-AA-010, Pre-Fire Plans, Revision
FP-AA-010, Pre-Fire Plans, Revision 1
FRH-II-531, HC PFP Diesel Generator Rooms, Revision 8
FRH-II-531, HC PFP Diesel Generator Rooms, Revision 8
FRH-II-541, Class 1E Switchgear Rooms 130' Elevation, Revision
FRH-II-541, Class 1E Switchgear Rooms 130 Elevation, Revision 7
FRH-II-562, HC PFP HVAC Equipment, Inverters and Batteries 163' Elevation, Revision 5
FRH-II-562, HC PFP HVAC Equipment, Inverters and Batteries 163 Elevation, Revision 5
FRH-III-151, HC PFP Turbine Building 137' Elevation, Revision 4
FRH-III-151, HC PFP Turbine Building 137 Elevation, Revision 4
FRH-III-321, Cable Tray Area and Battery Rooms 87' Elevation, Revision 5
FRH-III-321, Cable Tray Area and Battery Rooms 87 Elevation, Revision 5
MA-AA-734-497, General Instructions for Valve Packing, Revision 2
MA-AA-734-497, General Instructions for Valve Packing, Revision 2
Notifications
Notifications (*initiated in response to inspection)
(*initiated in response to inspection
20806786*
) 20806786* 20810330* 20810592* 20810740* 20813616* 20813616* 20424016 20598193 20611741 20629300 20684715 20722147 20723341 20723902 20745308 20775917 20791702 20791711 20791825 20791925 20791980 20792057 20793043 20793128 20793394 20796584 20803400 20803533 20803887 20812821 20816586 Maintenance Orders/Work Orders
20810330*
30325064 60106987 60111316 60122804 60131857 60140081 60140086 70069106 70153147 70165058 7018 5270 70185287 70200128 70200144 70200239 70201140 70201699 70202630 70204994 80122059 80122358 Miscellaneous
20810592*
20810740*
20813616*
20813616*
20424016
20598193
20611741
20629300
20684715
20722147
20723341
20723902
20745308
20775917
20791702
20791711
20791825
20791925
20791980
20792057
20793043
20793128
20793394
20796584
20803400
20803533
20803887
20812821
20816586
Maintenance Orders/Work Orders
30325064
60106987
60111316
60122804
60131857
60140081
60140086
70069106
70153147
70165058
70185270
70185287
200128
200144
200239
201140
201699
202630
204994
80122059
80122358
Miscellaneous
Hope Creek Fire Protection Completed Fire Drill List from 2016 through 2018
Hope Creek Fire Protection Completed Fire Drill List from 2016 through 2018
Hope Creek Fire Protection List of Outstanding Pre
Hope Creek Fire Protection List of Outstanding Pre-Fire Plan Revisions dated November 15,
-Fire Plan Revisions dated November 15, 2018 Hope Creek Fire Protection Night Order / Shift Communication dated October 31, 2018
2018
Hope Creek Troubleshooting Plan 16
Hope Creek Fire Protection Night Order / Shift Communication dated October 31, 2018
-056 Hope Creek Troubleshooting Plan 18
Hope Creek Troubleshooting Plan 16-056
-195
Hope Creek Troubleshooting Plan 18-195  
71153- Follow-Up of Events and Notices of Enforcement Discretion
 
71153-Follow-Up of Events and Notices of Enforcement Discretion
Procedures
Procedures
HC.OP-AB.BOP-0001, Feedwater Heating, Revision 20
HC.OP-AB.BOP-0001, Feedwater Heating, Revision 20
HC.OP-SO.AF-0001, Extraction Steam, Heating Vents and Drains System Operation, Revision 57 HC.OP-ST.GS-0003, Reactor Building/TORUS Vacuum Breaker Operability Test  
HC.OP-SO.AF-0001, Extraction Steam, Heating Vents and Drains System Operation,
- Monthly, Revision 9 Notifications
Revision 57
20814957 20815533 Maintenance Orders/Work Orders
HC.OP-ST.GS-0003, Reactor Building/TORUS Vacuum Breaker Operability Test - Monthly,
50195246 60141343
Revision 9
Notifications
20814957
20815533
Maintenance Orders/Work Orders
50195246
60141343
}}
}}

Latest revision as of 05:47, 5 January 2025

Integrated Inspection Report 05000354/2018004
ML19029A727
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 01/28/2019
From: Fred Bower
Reactor Projects Branch 3
To: Sena P
Public Service Enterprise Group
References
IR 2018004
Download: ML19029A727 (24)


Text

January 28, 2019

SUBJECT:

HOPE CREEK GENERATING STATION UNIT 1 - INTEGRATED INSPECTION REPORT 05000354/2018004

Dear Mr. Sena:

On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Hope Creek Generating Station (HCGS). On January 16, 2019, the NRC inspectors discussed the results of this inspection with Mr. Eric Carr, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one finding of very low safety significance (Green) in this report which involved a violation of NRC requirements. Further, inspectors documented a PSEG-identified violation which was determined to be of very low safety significance in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or the significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at HCGS. In addition, if you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC, 20555-0001; with copies to the Regional Administrator, Region I, and the NRC Resident Inspector at HCGS. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR ) Part 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Fred L. Bower, III, Chief Reactor Projects Branch 3 Division of Reactor Projects

Docket No.

50-354 License No.

NPF-57

Enclosure:

Inspection Report 05000354/2018004

Inspection Report

Docket Number:

50-354

License Number:

NPF-57

Report Number:

05000354/2018004

Enterprise Identifier: I-2018-004-0010

Licensee:

PSEG Nuclear LLC (PSEG)

Facility:

Hope Creek Generating Station (HCGS)

Location:

Hancocks Bridge, NJ 08038

Inspection Dates:

October 1, 2018 to December 31, 2018

Inspectors:

J. Hawkins, Senior Resident Inspector

S. Haney, Resident Inspector

J. Brand, Senior Reactor Inspector

J. DeBoer, Emergency Preparedness Inspector

J. Furia, Senior Health Physicist

T. Fish, Senior Operations Engineer

Approved By:

Fred L. Bower, III, Chief

Reactor Projects Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring PSEGs performance at

Hope Creek Generating Station (HCGS) Unit 1 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. NRC identified and self-revealed findings, violations, and additional items are summarized in the table below. Licensee-identified non-cited violations (NCVs) are documented in the following Inspection Results sections of the report: 7115

List of Findings and Violations

Inadequate High Pressure Coolant Injection Trip Unit Preventive Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Reactor Safety -

Mitigating Systems

Green NCV 05000354/2018004-01 Closed P.2 - Problem Identification and Resolution-Evaluation 71153 A Green self-revealing non-cited violation (NCV) of Technical Specification (TS) 6.8.1.a,

Procedures and Programs, was identified because PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units, which are circuit cards used in various emergency core cooling systems (ECCS) at HCGS. As a result, on September 26, 2018, a failure of the high pressure coolant injection (HPCI) system high water level trip unit occurred resulting in a blown fuse affecting the operability of HPCI and other A channel ECCS (Residual Heat Removal (RHR) and Core Spray). This resulted in PSEG entering a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shutdown Technical Specification Action Statement (TSAS)

(TS 3.5.1.c.2), an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> non-emergency report (EN#53625) for the HPCI system being inoperable, and a licensee event report (LER) for a condition that could have prevented the fulfillment of a safety function.

Additional Tracking Items

Type Issue number Title Inspection Results Section Status LER 05000354/2018-004-00 High Pressure Coolant Injection System Inoperable due to Failed Fuse 71153 Closed

PLANT STATUS

Hope Creek Generating Station (HCGS) began the inspection period at 100 percent rated thermal power (RTP). On December 6, 2018, Hope Creek reduced power to approximately 69 percent rated thermal power to support planned main turbine valve testing, control rod scram time and settle testing, control rod sequence exchange, and plant repairs, and returned to full power on December 8, 2018. There were no other operational power changes of regulatory significance for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess PSEG performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather (1 Sample)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to seasonal cold temperatures the week of November 26, 2018

71111.04 - Equipment Alignment

Partial Walkdown (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) C Emergency Diesel Generator (EDG) after the rocker arm lube oil tank was found with elevated moisture levels during the week of October 22, 2018
(2) A Primary Containment Instrument Gas (PCIG) system compressor after unsuccessful capacity test and troubleshooting the week of October 22, 2018
(3) B and C Station Service Water (SSW) with the A SSW pump out of service for planned maintenance on October 29, 2018
(4) Reactor protection system (RPS) relay missing sealant extent of condition inspections on December 12, 2018

71111.05AQ - Fire Protection Annual/Quarterly

Quarterly Inspection (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) C EDG room during the week of October 22, 2018
(2) B Variable Frequency Drive pump room during the week of October 29, 2018
(3) Auxiliary building Heating, Ventilation and Air Conditioning (HVAC), inverters and battery rooms during the week of November 1, 2018
(4) Auxiliary and service radwaste building cable tray and battery rooms during the week of November 15, 2018
(5) Auxiliary building switchgear rooms during the week of December 5, 2018

71111.06 - Flood Protection Measures

Internal Flooding (1 Sample)

The inspectors evaluated internal flooding mitigation protections in reactor auxiliaries cooling system room on November 8 and 9, 2018.

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

The inspectors observed and evaluated a crew of licensed operators in the plants simulator during licensed operator annual requalification operating examination that involved a reactor water cleanup pump trip, loss of the 10D410 125 volts direct current bus, high main turbine vibrations, a loss of offsite power and loss of coolant accident, and reactor vessel flooding on November 20, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated a planned down power to 69 percent rated thermal power to support planned main turbine valve testing, control rod scram time and settle testing, control rod sequence exchange, and plant repairs on December 6, 2018.

Operator Requalification Exam Results (Annual) (1 Sample)

The inspectors reviewed and evaluated requalification examination results (written and operating test) on December 21, 2018.

Operator Requalification Program and Operator Performance (Biennial) (1 Sample)

The inspectors reviewed and evaluated operator performance, evaluator performance, and simulator performance during the requalification examinations completed on December 19, 2018.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (2 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) High Pressure Coolant Injection (HPCI) trip unit failure on September 26, 2018
(2) Reactor Manual Control System transformer and power supplies failures during the week of November 6, 2018

71111.13 - Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unplanned A Electro-Hydraulic Control (EHC) pump replacement on October 15, 2018
(2) Planned open phase group B alarm and trip testing on November 28, 2018
(3) Planned A Standby Liquid Control (SLC) pump testing on November 29, 2018
(4) Planned single source of offsite power line-up during open phase testing and switchyard expansion from December 7 through 9, 2018

71111.15 - Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) D RHR minimum flow check valve chattering while performing the quarterly surveillance test on October 24, 2018
(2) B SSW pump discharge vent valve configuration control on November 12, 2018
(3) B and D EDG and HPCI transfer/isolation switch testing during the week of December 12, 2018

71111.18 - Plant Modifications

The inspectors evaluated the following temporary modifications:

(1) Temporary cooling of the B Reactor Recirculation Pump (RRP) seal purge line during the week of October 29, 2018
(2) Temporary rewiring of safety-related inverter fans during the week of November 5, 2018

71111.19 - Post Maintenance Testing

The inspectors evaluated post maintenance testing for the following maintenance/repair activities:

(1) PCIG compressor troubleshooting, relief valve repairs and retest on October 11, 2018
(2) Unplanned loss of the reactor manual control system following power supply replacements on October 30, 3018
(3) Planned air leak and troubleshooting of a scram dump valve during the week of December 7, 2018
(4) Emergent leak repair on the Reactor Water CleanUp (RWCU) regenerative heat exchanger on December 22, 2018

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Routine

(1) HC.OP-IS.BJ-0001, HPCI Main and Booster Set Inservice and 2-year Comprehensive Pump testing on December 4, 2018

Inservice (2 Samples)

(1) Review of HC-18-008, Relief Valve, Low-Low Set Channel Functional Test - Surveilance Test Interval (STI) Evaluation on October 31, 2018
(2) Review of HC-18-014, Control Room Emergency Filtration System Functional Test -STI Evaluation on October 31, 2018

Cornerstone: Emergency Preparedness

71114.04 Emergency Action Level and Emergency Plan Changes

The inspectors verified that the changes made to the emergency plan were done in accordance with 10 CFR 50.54(q)(3), and any change made to the Emergency Action Levels, Emergency Plan, and its lower-tier implementing procedures, had not resulted in any reduction in effectiveness of the Plan.

71114.06 - Drill Evaluation

Emergency Planning Drill (1 Sample)

The inspectors evaluated the conduct of a routine PSEG emergency planning drill on December 7,

RADIATION SAFETY

Cornerstone: Occupational and Public Radiation Safety

71124.01 Radiological Hazard Assessment and Exposure Controls

Contamination and Radioactive Material Control

The inspectors observed the monitoring of potentially contaminated material leaving the radiological controlled area and inspected the methods and radiation monitoring instrumentation used for control, survey, and release of that material.

High Radiation Area and Very High Radiation Area Controls

The inspectors reviewed the procedures and controls for High Radiation Areas, Very High Radiation Areas, and radiological transient areas in the plant.

71124.02 Occupational ALARA Planning and Controls

Radiological Work Planning

The inspectors selected the following radiological work activities based on exposure significance for review:

  • RWP 8, Refuel Floor Activities
  • RWP 10, Maintenance Support Activities
  • RWP 14, Drywell Maintenance Activities

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified PSEGs performance indicator submittals for Safety System Functional Failures from January 1, 2018, through December 29, 2018.

71152 - Problem Identification and Resolution

1. Semiannual Trend Review (1 Sample)

The inspectors reviewed PSEGs corrective action program for trends that might be indicative of a more significant safety issue.

2. Annual Follow-up of Selected Issues (1 Sample)

The inspectors reviewed PSEGs implementation of its corrective action program (CAP)related to the following issues:

(1) NOTF 20791702, HPCI Warm-up line bypass line isolation valve (F100) excessive package leakage during the week of November 26, 2018

===71153 - Follow-up of Events and Notices of Enforcement Discretion

1. Events

=

The inspectors evaluated PSEGs response during the following non-routine evolutions and transients:

(1) Trip of the 5C feedwater heater on December 12, 2018
(2) Safety Relief Valve (SRV) main seat leakage causing condensate induced water hammer and noises in the discharge line to the torus identified on December 20, 2018

2. Licensee Event Reports (1 Sample)

The inspectors evaluated the following LER, which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000354/2018-004-00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, dated November 20, 2018 (ADAMS Accession: ML18324A614). The circumstances surrounding this LER are documented in the Inspection Results section of this report.

INSPECTION RESULTS

Licensee Identified Non-Cited Violation 71152 This violation of very low safety significant was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Hope Creek Generating Station Renewed Facility Operating License No. NPF-57, Condition 2.C.15.b.3 requires, in part, that no disbursements or payments from the

[decommissioning] trust shall be made by the trustee until the trustee has first given the NRC 30 days notice of the payment.

Contrary to the above, on occasions between 2001 and 2015, disbursements from the Hope Creek Generating Station decommissioning trust were made by the trustee and the trustee had not first given the NRC 30 days notice of the payment. Specifically, in 2001, 2012, and 2015, PSEG directed the Bank of New York Mellon (the trustee of the decommissioning trust for Hope Creek Generating Station) to disburse payments equaling $240,449.04 for decommissioning cost estimates. However, PSEG failed to notify the NRC of these disbursements until October 19, 2018 (ML18295A023).

Significance/Severity: This issue is considered within the traditional enforcement process because the failure to inform the NRC prior to disbursing decommissioning funds impacts the ability of the NRC to perform its regulatory oversight function. As noted in Section 2.2.4 of the NRC Enforcement Policy, such violations are dispositioned using traditional enforcement.

The inspectors evaluated the violation in accordance with the NRC Enforcement Policy and determined that it is appropriately characterized at Severity Level IV (SL IV) because it is similar to the SL IV example violation 6.9.d.7, describing a licensees failure to provide or make a 15-day or 30-day written report or notification that does not impact the regulatory response by the NRC. For this Hope Creek issue, the inspectors determined that the disbursements were made for acceptable decommissioning expenses and would not have necessitated further inquiry or caused the NRC to object to the payments.

Corrective Action Reference: Notification (NOTF) 20808984

Minor Violation 71152

(1) Minor Violation: During the review of NOTFs written for fire protection activities, the inspectors identified multiple pre-fire plans (PFPs) that were inadequate as well as 29 other PFPs that had been awaiting revision for up to 13 years. The inspectors determined that PSEG not maintaining current, detailed, and accurate PFPs available to the fire brigade was contrary to the HCGS license condition, the Updated Final Safety Analysis Report, and PSEGs implementing procedures and was a performance deficiency within their ability to foresee and correct and which should have been prevented.

Screening: The inspectors evaluated the issue above in accordance with the guidance in the NRCs Enforcement Policy, IMC 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues, and determined the issue was a minor violation because, although PSEG was not maintaining current, detailed and accurate PFPs, this deficiency did not significantly impact the fire brigades ability to fight a fire in the affected fire areas.

Enforcement:

PSEG has taken actions to restore compliance by documenting additional NOTFs to revise the inaccurate PFPs identified by the inspectors, as well as planning/scheduling the completion of all revisions to every PFP by January 2019.

PSEG did not comply with HCGS License Condition 2.C.(7) which requires PSEG to implement and maintain in effect all provisions of the approved fire protection program as described in the UFSAR Section 9.5.1.5.3 and Appendix 9A.III.K for Administrative Controls states, in part, that Pre-fire plans are written for all safety-related areas. Fire Protection Program implementing procedure FP-AA-010, Pre-Fire Plans, requires, in part, that pre-fire plans shall be established for all safety-related areas and areas representing a hazard to safety-related equipment. The procedure also requires that the station establish a formal tracking mechanism to ensure that the pre-fire plans are reviewed and updated as necessary. FP-AA-010 also states that the fire protection supervisor/fire marshal is responsible for ensuring the pre-fire plans are current, including the performance of periodic reviews and updates, as necessary. This constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy.

Observations 71152

(1) Corrective Action Program (CAP) Evaluations NRC Inspection Reports (IRs) 2017004 and 2016004, Sections 40A2.2, documented the inspectors Semi-Annual Trend reviews of historical CAP evaluations performed each year since 2013. Since 2017, PSEG has implemented the industry initiatives to improve the effectiveness of issue resolution to enhance safety and efficiency within their CAP and the inspectors summarized the CAP data trend below:

Summarized HCGS CAP Information

2016 (RFO)2017 2018 (RFO)

RCEs

ACEs

CCEs

WGEs

Evaluation Totals:

CA Totals:

324*

197 333*

Note:

  • designate RFO was performed during the calendar year.

PSEGs total number of CAP evaluations reduced by approximately 50 percent from 2016 to 2017 and remained approximately the same from 2017 to 2018. Although the number of evaluations dropped, the inspectors noted the number of corrective actions remained consistent over the last three years (when considering the difference between refueling outage (RFO) years and non-RFO years).

Issue Identification, Evaluation and Resolution The inspectors evaluated a number of notifications generated over the course of the past two quarters by departments that provide input to the quarterly trend reports. The inspectors determined that, in most cases, issues were appropriately evaluated by PSEG staff for potential trends and resolved within the scope of the CAP. Examples of this are documented below:

1) FLEX Equipment Reliability and Preventive Maintenance In NRC IR 2018002, the Semi-Annual Trend review section documented an increase in FLEX equipment and preventive maintenance issues. PSEG completed a common cause evaluation (70201140) to address the inspectors previous concerns about the potential adverse trend, and over the past two quarters there has been a reduction in identified FLEX issues. The FLEX engine control module (ECM) and heater relay failures were addressed by the site replacing all of these components on the susceptible equipment and conducting failure analyses on the failed components. (See NOTFs 20800028, 20796584, 20799580, 20803195, and Order 70201699)

2) Relay Replacements in the Reactor Protection System During an RF21 RPS relay replacement, the inspectors identified that the relay did not have the required fire protection sealant used as a separation barrier inside of the RPS cabinet. PSEG documented the condition in NOTF 20798788 on June 20, 2018, and NOTF 20800461 on July 18, 2018. The inspectors tracked PSEGs completion of the extent of condition regarding other RPS relays which was performed in December 2018, with no additional deficiencies noted.

However, the inspectors noted a few instances where PSEG was not timely or did not recognize, until prompted by the inspectors, that potential adverse trends existed. Examples of this are documented below:

1) SRV Main Seat Leakage In NRC IR 2018002, the Semi-Annual Trend review section documented multiple high SRV tailpipe temperatures and conclusions that two of these SRVs, H and K, were exhibiting signs of main seat leakage. Then, in NRC IR 2018003, an annual sample conducted for H SRV and D MSL issues documented that on September 5, 2018. On that date, PSEG also initiated NOTF 20803213 recommending that engineering review the conclusions and corrective actions from a 2014 causal evaluation (ACE 70168360) due to the inspectors questions. Upon further review, the inspectors noted that PSEG had not taken action on NOTF 20803213 because even though there was automatic relief valve seat leakage it had not progressed and begun generating cyclic noises associated with condensate induced water hammer. In 2014, these noises associated with condensate induced water hammer occurred in the torus approximately ~20 times/min. October 1, 2018, the inspectors noted that PSEG initiated NOTF 20806044 for degrading conditions associated with the H SRV main leakage, and then documented the reoccurrence of the condensate induced water hammer in the torus in NOTF 20814836 on December 20, 2018. As of December 31, 2018, PSEG initiated actions to develop an adverse condition monitoring (ACM) plan and operation technical decision making (OTDM) document for the issue. In addition, PSEG initiated NOTF 20816775 when the inspectors determined that the H SRV main seat leak rate data from August to December 2018 was incorrect and did not include peer checks.

2) Fire Drills The inspectors noted during their review that in the last 3 years there has only been one fire drill conducted inside the RCA and that there few variations on fire drill locations. The inspectors observed that the purpose of these fire drills per, FP-AA-014, Fire Protection Training Program, is to assess the readiness of the fire brigade and the adequacy of the fire-fighting strategies, procedures and PFPs. PSEG acknowledged and documented in NOTF 20815151 the need to vary the location of fire drills and to revise PFPs in a timely manner.

3) Review of Operating Experience (OE) and Vendor Technical Information The inspectors noted an increase in NOTFs written to address gaps in PSEGs use and review of operating experience and untimely updates to vendor technical information.

(See NOTFs 20802555, 20801537, 20801634, 20800447, 20803032, 20800510, 20802580, 20801654, 20802392, and 702022203.)

The inspectors evaluated all of the issues above in accordance with the guidance in IMC 0612, Appendix B, Issue Screening, and Appendix E, Examples of Minor Issues, and determined the issues were of minor significance because the inspectors did not identify any CAQs that were not appropriately corrected or scheduled for correction in a reasonable period of time as a result of the failure to implement the NOTF screening process appropriately.

Consequently, these issues were not subject to enforcement action in accordance with the NRCs enforcement policy.

Observation 71152 (2.1)

The inspectors reviewed PSEGs corrective actions regarding excessive packing leakage from the HPCI warm-up valve (HD-F-100) during the last operating cycle. PSEG initiated corrective action notification 20791702 on April 3, 2018, and performed an Equipment Reliability Evaluation (RE-70200144). PSEG determined the two causes were low packing gland stress and severe valve stem pitting corrosion. The inspectors reviewed this valves historical packing leaks, past operability and reportability evaluations, maintenance rule applicability and effects on performance indicators associated with this issue. The inspectors determined that PSEG conducted an appropriate review of the issue, including an adequate extent of condition review and had implemented timely corrective actions to address the causes of the excessive packing leak. The inspectors noted that PSEG had documented packing leaks on this valve on the last four operating cycles going back to 2013. However, the inspectors could not find documentation to show that a corrective action initiated for a June 12, 2013, excessive packing leak under maintenance work order 60111316 to inspect the valve stem for pitting or damage was properly implemented. The inspectors determined this was a missed corrective action opportunity to identify the degraded valve stem for a problem that has since been corrected. The inspectors determined this performance deficiency was minor because the repeated packing leaks did not impact operability of the valve or HPCI system or any other safety related components and did not require an unplanned power reduction or plant shutdown to implement repairs.

Trip Unit Inadequate Preventive Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Reactor Safety - Mitigating Systems

Green NCV 05000354/2018004-01 Closed P.2 - Problem Identification and Resolution

- Evaluation 71153 (2.1)

A Green self-revealing NCV of TS 6.8.1.a, Procedures and Programs, was identified because PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units, which are circuit cards used in various ECCS at HCGS. As a result, on September 26, 2018, a failure of the HPCI system high water level trip unit occurred resulting in a blown fuse affecting the operability of HPCI and other A channel ECCS (RHR and CS). This resulted in PSEG entering a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shutdown TSAS (TS 3.5.1.c.2), an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> non-emergency report (EN 53625) for the HPCI system being inoperable, and an LER for a condition that could have prevented the fulfillment of a safety function.

Description:

HGCS utilizes over 200 individual Rosemount trip modules in 42 functional locations throughout the plant, mainly in the reactor protection, reactor recirculation, and ECCS. The HPCI trip logic is performed by these Rosemount trip units as they are arranged in card files containing multiple units which share a common fuse.

On September 26, 2018, while operating at 100 percent power, PSEG received indications in the main control room that the HPCI system had become inoperable due to a failed fuse in channel A of the system initiating logic. This failed fuse also affected the A channel of the core spray and LPCI sub-systems. PSEGs immediate investigation isolated the fuse failure to a single component, a Rosemount trip unit, associated with the HPCI system high water level trip (level 8). With the fault isolated by PSEGs troubleshooting, operability was restored to the affected A channel ECCS after being in a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shutdown TS for 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. PSEG restored HPCI system operability by replacing the failed trip unit on September 27, 2018. As a result, PSEG reported this as a condition that could have prevented the fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(D) to the NRC as LERs 05000354/2018-004-00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, on November 20, 2018.

On December 11, 2018, PSEG completed a causal evaluation (ERE 70203043) for the failed HPCI trip unit. This evaluation determined that the C25 capacitor in the Rosemount slave trip unit, model 510DU7, failed after being installed in the plant for 32 years (manufactured

~39 years ago). PSEG concluded that even though a Part 21 on these C25 capacitors failing had been issued in 1999, this failure was random due to the low frequency of occurrence in the industry and at HCGS. PSEGs corrective actions included replacing the failed trip unit and associated fuse, conducting a failure analysis on the failed trip unit, creating actions to implement a trip unit reliability strategy (either to replace all or replace selected trip units) as recommended by the circuit card performance team and plant health committee (PHC).

The inspectors reviewed PSEGs evaluation and questioned PSEG about the Part 21 issued in 1999. Rosemount had issued the Part 21 (1999-31-0) for failures of the C25 capacitor on trip units manufactured prior to date code 8630 (week 30 of 1986). The Part 21 recommended further examination to determine if pre-8630 capacitors were installed and whether or not replacement was warranted. The inspectors noted that PSEGs follow-up actions for the Part 21 reviewed under CR990624091 were to inspect and repair the trip units in stock. These actions were put into PSEGs corrective action program under 60012450, 80002672, and 20042758, but were never completed.

The inspectors then questioned PSEGs review and implementation of the Circuit Card - Rosemount Trip Unit preventive centered maintenance (PCM) template. PSEG initially performed a PCM template evaluation for Rosemount trip units in 2009 (Order 70083963) and then due to PCM template revisions, re-reviewed their own maintenance strategy and their justification in 2015 (70157122, 70162269, 70172811) and 2017 (70169938). The PCM template recommended replacement of the 510DU7 and 710DU trip units on an 18 year frequency. Although this maintenance strategy was approved by PSEGs PHC in 2009, PSEG did not approve funding citing the potential large expense and low failure rate of the units over the life of the plant. PSEGs conclusion in 2009, was re-evaluated in 2015 and 2017, with no additional justification for the decision. PSEG did not create preventive maintenance activities for the replacement of selected trip units based on the risk associated with the trip units failure.

The inspectors reviewed the most recent PCM template revision for Circuit Card - Rosemount Trip Units from October 2014. This revision was reviewed by PSEG under 2014 NOTF 20664484 and 2017 Order 70169938 which cut, copied, and pasted the 2009 PCM template evaluation under 2009 Order 70083963

(09) which recommends replacement or refurbishment of the model 510DU7 trip units on a 12 year frequency. The PCM template also states that the maximum replacement frequency for any critical card should be 30 years. And that the 30 year maximum attempts to limit the vulnerability of the plant to circuit card failures from the long term effects of corrosion, vibration, trace degradation, and all of a circuit cards failure mechanisms.

Also, the inspectors found that up until February 2018, PCM template implementation evaluations were performed using Section 4.14 of PSEG procedure MA-AA-716-210-1001.

Section 4.14.9 requires compilation of information necessary to evaluate the PCM template recommendations, including external documents and industry operating experience (OPEX).

PSEGs own OPEX search that was conducted as part of their causal evaluation (ERE 70203043) yielded 4 distinct recent events involving the failure of a C25 capacitor on a Rosemount trip unit that resulted in impacts to other safety-related systems and entry into short duration shutdown TSASs (NMP 16, Perry 13 & 10, Limerick 09). PSEG procedure MA-AA-716-210 (now ER-AA-210), Preventive Maintenance (PM) Program, Section 4.2.4 PCM Template Process, states that all PMs that deviate from the PCM template recommendations require a justification documented in the PM Change Process.

Because of this, the inspectors determined that the justification used by PSEG to not implement a replacement frequency for their Rosemount trip units in 2017, was inadequate because it did not address the revised replacement/refurbishment frequency of 12 years for the Rosemount trip units, the maximum recommended replacement frequency of 30 years for any critical circuit card, or recent industry operating experience involving similar trip unit failures.

Corrective Actions: PSEGs corrective actions included replacing the failed trip unit and associated fuse, conducting a failure analysis on the failed trip unit, and creating actions to implement a trip unit reliability strategy (either to replace all or replace selected trip units) as recommended by the circuit card performance team and plant health committee (PHC)..

Corrective Action Reference: 20806069.

Performance Assessment:

Performance Deficiency: PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the Rosemount trip units. This represented a performance deficiency that was reasonably within the licensees ability to foresee and correct and should have been prevented.

Screening: The performance deficiency was determined to be more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone, and adversely affected the cornerstone to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, in this case, because PSEG did not adequately justify the replacement frequency for the trip units which resulted in the loss of safety related ECCS equipment, loss of RPS redundancy, and entry into a short duration shutdown TSAS.

Significance: The inspectors determined that this finding was of very low safety significance (Green) using NRC IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2 - Mitigating Systems Screening Questions, dated July 1, 2012, because the finding did not represent a loss of system and/or function, did not represent an actual loss of function of at least a single train for greater than its TS allowed outage time or an actual loss of function of one or more non-TS trains of equipment designated as high safety-significant in accordance with PSEGs maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Cross-Cutting Aspect: This finding is related to the cross-cutting area of Problem Identification and Resolution, Evaluation, because PSEG did not thoroughly evaluates issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, the inspectors determined that PSEG did not thoroughly re-evaluate the PM replacement justification for safety-related Rosemount trip units in 2017.

(P.2)

Enforcement:

Violation: TS 6.8.1.a, Procedures and Programs, requires in part, that written procedures recommended in Appendix A of Regulatory Guide (RG) 1.33, Revision 2, shall be established, implemented, and maintained. Section 9 of RG 1.33, Revision 2, Appendix A, recommends procedures for performing maintenance, including: a. maintenance that can affect the performance of safety-related equipment should be properly pre-planned and performed in accordance with written procedures and documented instructions appropriate to the circumstances; and, b. preventive maintenance schedules should be developed to specify the inspection or replacement of parts that have a specific lifetime. In 2017, PSEGs procedure MA-AA-716-210-1001 for PCM template implementation evaluations details the implementation evaluation process which formally documents and justifies PSEGs approved maintenance strategies.

Contrary to the above, between 2009 and 2017, PSEG did not adequately establish, implement, and maintain the initial replacement frequency for the for Rosemount trip units, which are circuit cards used in various ECCS at HCGS. As a result, on September 26, 2018, a failure of the HPCI system trip unit occurred resulting in a blown fuse affecting the operability of both HPCI and A channel ECCS. This resulted in PSEG entering a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shutdown Technical Specification, an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> non-emergency report for the HPCI system being inoperable, and an LER for a condition that could have prevented the fulfillment of a safety function. PSEGs corrective actions included replacing the failed trip unit and associated fuse and creating actions to implement a trip unit reliability strategy.

Disposition: This violation is being treated as an NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On November 29, 2018 the inspector presented the inspection results of PSEGs implementation of its corrective action program related to the HPCI warmup valve excessive to Tanya Timberman, Regulatory Compliance. The inspectors verified no propertiety information was retained or documented in this report.
  • On November 30, 2018, the inspector presented the radiation safety inspection results to H. Trimble, Radiation Protection Manager, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.
  • On January 16, 2019, the inspectors presented the quarterly resident inspector inspection results to Mr. Eric Carr, Site Vice President, and other members of the PSEG staff.

THIRD PARTY REVIEWS

The inspectors reviewed Institute of Nuclear Power Operations reports that were issued during the inspection period.

Observation 71153 (2.1)

Licensee Event Report 05000354/2018-004-00: High Pressure Coolant Injection System Inoperable due to Failed Fuse

On September 26, 2018, while operating at 100 percent power, PSEG received indications in the main control room that the HPCI system had become inoperable due to a failed fuse in channel A of the system initiating logic. This failed fuse also affected the A channel of the core spray and LPCI sub-systems. PSEGs investigation isolated the fuse failure to a single component, a Rosemount trip unit, associated with the HPCI system high water level trip (level 8). With the fault isolated, operability was restored to the affected A channel emergency core cooling systems. PSEG restored HPCI system operability by replacing the failed trip unit on September 27, 2018. As a result, PSEG reported this to the NRC as a condition that could have prevented the fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(D) as LER 05000354/2018-004-00, High Pressure Coolant Injection System Inoperable due to Failed Fuse, on November 20, 2018. The inspectors performed inspections documented in the Maintenance Effectiveness (71111.12) and Performance Indicator Verification (71151) Sections of this report. The inspectors identified a performance deficiency during the review of this LER and related inspections of the Rosemount trip unit that is documented below. This review closes LER 05000354/2018-004-00.

DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

HC.OP-AB.MISC-0001, Acts of Nature, Revision 33

HC.OP-GP.ZZ-0003, Station Preparations for Winter Conditions, Revision 31

Notifications

20810731

20811656

20811719

20811837

20811932

20811933

20811934

20813248

Section 1R04: Equipment Alignment

Procedures

HC.OP-FT.KL-0001, Primary Containment Instrument Gas System Comprehensive Capacity

Test, Revision 1

HC.OP-ST.KJ-0003, Emergency Diesel Generator 1CG400 Operability Test, Revision 77

Notifications

20798788

20802492

20803055

20803058

20812962*

Maintenance Orders/Work Orders

60139934

60140087

202651

Section 1R05: Fire Protection

Procedures

AD-AA-101-1005, Procedure Revision Priority Coding and Expectations, Revision 1

FP-AA-010, Pre-Fire Plans, Revision 1

FRH-II-531, HC PFP Diesel Generator Rooms, Revision 8

FRH-II-541, Class 1E Switchgear Rooms 130 Elevation, Revision 7

FRH-II-562, HC PFP HVAC Equipment, Inverters and Batteries 163 Elevation, Revision 5

FRH-III-151, HC PFP Turbine Building 137 Elevation, Revision 4

FRH-III-321, Cable Tray Area and Battery Rooms 87 Elevation, Revision 5

Notifications (*initiated in response to inspection)

20810330*

20810592*

20810740*

20424016

20629300

20803887

20812821

20814931

20816586

Maintenance Orders/Work Orders

60141360

70153147

204994

80122358

Miscellaneous

Hope Creek Fire Protection Completed Fire Drill List from 2016 through 2018

Hope Creek Fire Protection Night Order / Shift Communication dated October 31, 2018

Hope Creek Fire Protection List of Outstanding Pre-Fire Plan Revisions dated

November 15, 2018

Section 1R06: Flood Protection Measures

Procedures

HC.OP-ST.EA-0002, Service Water System Functional Test - 18 Months, Revision 5

Maintenance Orders/Work Orders

50185261

50189406

50190174

Miscellaneous

HC-PRA-012, Hope Creek Generating Station Probabilistic Risk Assessment Internal Flood

Notebook, Revision 3

Section 1R11: Licensed Operator Requalification Program

Miscellaneous

ESG-015, RWCU Pump Trip, Loss of 10D410, Turbine Vibrations, LOP/LOCA, Rx Flooding,

dated November 7, 2018

Section 1R12: Maintenance Effectiveness

Procedures

ER-AA-210, Preventive Maintenance (PM) Program, Revision 0

ER-AA-310-1002, Maintenance Rule - SSC Risk Significance Determination, Revision 7

ER-AA-600-1015, FPIE PRA Model Update, Revision 8

ER-AA-600-1044, Maintenance Rule Support, Revision 5

HC-MRULE-001, HCGS Probabalistic Risk Assessment - HC Maintenance Rule Risk

Significance Catergorization, Revision 3

LS-AA-115, Operating Experience Program, Revision 16

MA-AA-716-210-1001, Performance Centered Maintenance (PCM Templates), Revision 13

Notifications

20808273

20808338

20809870

20810854

Maintenance Orders/Work Orders

60140456

70083963

70157122

70162269

70172811

203043

204092

Miscellaneous

HC Troubleshooting Plan 18-168

MTG-2018-00212

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

HC.OP-FT.KJ-0003, Emergency Diesel Generator 1CG400 - Functional Test, Revision 9

HC.OP-IS.BH-0003, Standby Liquid Control Pump AP208 - Inservice Test, Revision 16

OP-HC-108-115-1001, Operability Assessment and Equipment Control Program, Revision 36

WC-AA-101, On-line Work Management Process, Revision 25

Notifications (*initiated in response to inspection)

20807472*

20777837

20779618

20784239

20794566

20794567

20794715

20798272

20798273

20800410

20807066

20807078

20807499

20807625

Maintenance Orders/Work Orders

30322641

60139612

60139613

70197036

Miscellaneous

Hope Creek Generating Station On-Line Risk Assessment, Work Week 842, Applicable Period

10/14/18 - 10/20/18, Revision 0

Hope Creek Generating Station On-Line Risk Assessment, Work Week 842, Applicable Period

10/14/18 - 10/20/18, Revision 1

Section 1R15: Operability Determinations and Functionality Assessments

Procedures

HC.IC-CC.BB-0062, Nuclear Boiler - Division 4 Channel B21-N707D Safety Relief Valve

B21-F013P Low-Low Set, Revision 9

HC.IC-FT.BB-0073, Channel A - CS, HPCI, RHR, PCIS Rosemount Trip Units, Revision 6

HC.OP-IS.BC-0104, Residual Heat Removal Subsystem D Valves - Inservice Test, Revision 28

HC.OP-IS.BF-0101, Control Rod System Valves - Inservice Test, Revision 21

OP-AA-108-101-1002, Component Configuration Control, Revision 11

Notifications

20734665

20756667

20772331

20800262

20801704

20806153

20808531

20811707

Maintenance Orders/Work Orders

229368

50183099

50194371

50197720

50199947

202024

204029

204150

204881

205499

205829

206068

60138614

60139795

70195608

Section 1R18: Plant Modifications

Procedures

HC.OP-AB.RPV-0003, Recirculation System/Power Oscillations, Revision 32

Notifications

20793755

20795331

20795496

20796552

20801395

Maintenance Orders/Work Orders

80122350

80122499

Miscellaneous

TCCP 4HT-13-008, Temporary Cooling for the Recirculation Pump Seal Purge Line

TCCP 4HT-18-012, Temporary Cooling for the Recirculation Pump Seal Purge Line

Section 1R19: Post-Maintenance Testing

Procedures

HC.OP-FT.KL-0001, Primary Containment Instrument Gas System Compressor Capacity Test,

Revision 1

Notifications

20769194

20802492

20808273

20808338

20816502

20816638

Maintenance Orders/Work Orders

266260

60135779

60135861

60140047

60140456

60141422

80124125

Section 1R22: Surveillance Testing

Procedures

ER-AA-450, Implementation of the Technical Specification Surveillance Frequency Control

Program, Revision 2

HC.OP-IS.BJ-0002, HPCI Jockey Pump - AP228 - Inservice Test, Revision 35

LS-AA-106-101, Station Review Committee, Revision 0

Notifications

20743957

20803682

Maintenance Orders/Work Orders

30326348

50192426

50194073

206595

Miscellaneous

HC-14-014, Control Room Emergency Filtration System Functional Test STI Evaluation,

Revision 0

HC-18-008, Relief Valve, Low-Low Set Channel Functional Test Surveillance Test Interval (STI)

Evaluation, Revision 0

HC-STI-022, Risk Evaluation of Surveillance Interval Extension for Low-Low Set SRV

Operability Test, Revision 0

HC-STI-027, Risk Evaluation of Control Room Emergency Filtration System Functional Test,

Revision 0

Hope Creek Lubricating Oil Report for H1FD-10-S-211 dated October 10, 2018

Section 1EP4: Emergency Action Level and Emergency Plan Changes

Miscellaneous

2018-02, OP-AA-101-111, Roles and Responsibilities of On Shift Personnel, Revision 10

2018-21, 80111425 - 2R19A-D Steam Generator Blowdown Radiation Monitors

2018-24, NC.EP-EP.ZZ-0309 Dose Assessment (MIDAS) Instructions Revision 16

2018-56, Emergency News Center as Backup Emergency Operations Facility

Section 1EP6: Drill Evaluation

Procedures

EP-AA-125-1002, NRC Drill and Exercise Performance (DEP) Indicator Guidance, Revision 5

EP-HC-111-131, Hope Creek Wall Chart (Hot), Revision 1

Section 4OA1: Performance Indicator Verification

Procedures

LS-AA-2001, Collecting and Reporting of NRC Performance Indicator Data, Revision 11

LS-AA-2080, Monthly Data Elements for NRC Safety System Functional Failures, Revision 5

Notifications

20791702

20793327

20795822

20799118

20804677

Miscellaneous

Licensee Event Report 2018-004-00, HPCI System Inoperable due to Failed Fuse dated

November 20, 2018

Section 4OA2: Problem Identification and Resolution

Procedures

AD-AA-101-1005, Procedure Revision Priority Coding and Expectations, Revision 1

FP-AA-010, Pre-Fire Plans, Revision 1

FRH-II-531, HC PFP Diesel Generator Rooms, Revision 8

FRH-II-541, Class 1E Switchgear Rooms 130 Elevation, Revision 7

FRH-II-562, HC PFP HVAC Equipment, Inverters and Batteries 163 Elevation, Revision 5

FRH-III-151, HC PFP Turbine Building 137 Elevation, Revision 4

FRH-III-321, Cable Tray Area and Battery Rooms 87 Elevation, Revision 5

MA-AA-734-497, General Instructions for Valve Packing, Revision 2

Notifications (*initiated in response to inspection)

20806786*

20810330*

20810592*

20810740*

20813616*

20813616*

20424016

20598193

20611741

20629300

20684715

20722147

20723341

20723902

20745308

20775917

20791702

20791711

20791825

20791925

20791980

20792057

20793043

20793128

20793394

20796584

20803400

20803533

20803887

20812821

20816586

Maintenance Orders/Work Orders

30325064

60106987

60111316

60122804

60131857

60140081

60140086

70069106

70153147

70165058

70185270

70185287

200128

200144

200239

201140

201699

202630

204994

80122059

80122358

Miscellaneous

Hope Creek Fire Protection Completed Fire Drill List from 2016 through 2018

Hope Creek Fire Protection List of Outstanding Pre-Fire Plan Revisions dated November 15,

2018

Hope Creek Fire Protection Night Order / Shift Communication dated October 31, 2018

Hope Creek Troubleshooting Plan 16-056

Hope Creek Troubleshooting Plan 18-195

71153-Follow-Up of Events and Notices of Enforcement Discretion

Procedures

HC.OP-AB.BOP-0001, Feedwater Heating, Revision 20

HC.OP-SO.AF-0001, Extraction Steam, Heating Vents and Drains System Operation,

Revision 57

HC.OP-ST.GS-0003, Reactor Building/TORUS Vacuum Breaker Operability Test - Monthly,

Revision 9

Notifications

20814957

20815533

Maintenance Orders/Work Orders

50195246

60141343