IR 05000247/2010004: Difference between revisions

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{{Adams|number = ML103120352}}
{{Adams
| number = ML103140355
| issue date = 11/10/2010
| title = IR 05000247-10-004, on 07/01/2010 - 09/30/2010, Indian Point Nuclear Generating, Indian Point, Unit 2, Post-Maintenance Testing
| author name = Lew D C
| author affiliation = NRC/RGN-I/DRP/PB2
| addressee name = Pollock J E
| addressee affiliation = Entergy Nuclear Operations, Inc
| docket = 05000247
| license number = DPR-026
| contact person = Gray, Mel NRC/RGNI/DRP/PB2/610-337-5209
| case reference number = EA-10-212
| document report number = IR-10-004
| document type = Inspection Report, Letter
| page count = 37
}}


{{IR-Nav| site = 05000247 | year = 2010 | report number = 004 }}
{{IR-Nav| site = 05000247 | year = 2010 | report number = 004 }}


=Text=
=Text=
{{#Wiki_filter:UNITED NUCLEAR REGULATORY REGION 475 ALLENDALE KING OF PRUSSIA, PA November 8, 2010 Mr. Joseph Site Vice President Entergy Nuclear Operations, Inc. Indian Point Energy Center 450 Broadway, GSB Buchanan, NY 10511-0249 INDIAN POINT NUCLEAR GENERATING UNIT 3 -NRC INTEGRATED INSPECTION REPORT 05000286/2010004
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406*1415 November 10. 2010 EA-10-212 Mr. Joseph Site Vice President Entergy Nuclear Operations, Inc. Indian Point Energy Center 450 Broadway, GSB Buchanan, NY 105110249 INDIAN POINT NUCLEAR GENERATING UNIT 2 -NRC INTEGRATED INSPECTION REPORT 05000247/2010004 AND EXERCISE OF ENFORCEMENT DISCRETION


==Dear Mr. Pollock:==
==Dear Mr. Pollock:==
On September 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 3. The enclosed integrated inspection report documents the inspection results, which were discussed on October 28, 2010 with you and other members of your staff. The inspection examined activities conducted under your license as they reljite to safety and compliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. This report documents one self-revealing finding of very low safety significance (Green). This finding was determined to involve a violation of NRC requirements. However, because of the very low safety significance and because it is entered into your corrective action program (CAP), the NRC is treating it as a non-cited violation (NCV) consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATrN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region 1; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 3. In addition, if you disagree with the cross-cutting aspect assigned to the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region 1, and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 3. In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC PubliC Document Room of from the Publicly Available Records component of the NRC's document system (ADAMS).
On September 30,2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report documents the inspection results, which were discussed on October 28, 2010, with you and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


J. 2 ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).
This report documents one self-revealing finding of very low safety significance (Green). This finding was determined to involve a violation of NRC reqUirements.


Sincerely. /vIJAv-y-' Mel Gray, Chief Projects Branch 2 Division of Reactor Projects Docket No. 50-286 License No. DPR-26 Inspection Report No. 05000286/2010004 wI  
However, because of its very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. Additionally, if you disagree with the cross-cutting aspect assigned to the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. r I In addition, the inspectors reviewed Licensee Event Report 05000247/2010-004, which described the circumstances associated with reactor coolant system pressure boundary leakage from a five-sixteenth inch through-wall weld defect located at a socket weld associated with the 22 reactor coolant pump three-quarter inch seal bypass line. Although this issue constitutes a violation of NRC requirements, in that any reactor coolant system boundary leakage at power constitutes a violation, the NRC concluded that this issue was not within Entergy's ability to foresee and correct, that Entergy staff's actions did not contribute to the degraded condition, and that actions taken were reasonable to identify and address this matter. As a result, the NRC did not identify a performance deficiency.
 
A risk evaluation was performed and the issue was determined to be of very low safety significance.
 
Based on these facts, I have been authorized, after consultation with the Director, Office of Enforcement, and the Regional Administrator, to exercise enforcement discretion in accordance with Section 3.5 of the Enforcement Policy and refrain from issuing enforcement for the violation.
 
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of from the Publicly Available Records component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room). David C. Lew, Director DiviSion of Reactor Projects Docket No. 50*247 License No. DPR-26  
 
===Enclosure:===
Inspection Report No. 05000247/2010004 wI  


===Attachment:===
===Attachment:===
Supplemental Information cc Distribution via ListServ J. 2 ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).
Supplemental Information cc w/encl: Distribution via ListServ Enclosure J. 2 In addition, the inspectors reviewed licensee Event Report which described the circumstances associated with reactor coolant system pressure boundary leakage from a five-sixteenth inch weld defect located at a socket weld associated with the 22 reactor coolant pump inch seal bypass line. Although this issue constitutes a violation of NRC requirements, in that any reactor coolant system boundary leakage at power constitutes a violation, the NRC concluded that this issue was not within Entergy's ability to foresee and correct, that Entergy staffs actions did not contribute to the degraded condition, and that actions taken were reasonable to identify and address this matter. As a result, the NRC did not identify a performance deficiency.
 
A risk evaluation was performed and the issue was determined to be of very low safety significance.
 
Based on these facts, I have been authorized, after consultation with the Director, Office of Enforcement, and the Regional Administrator, to exercise enforcement discretion in accordance with Section 3.5 of the Enforcement Policy and refrain from issuing enforcement for the violation.
 
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of from the Publicly Available Records component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at Public Electronic Reading Room).
 
Sincerely,IRA! David C. Lew, Director Division of Reactor Projects Docket No.


Sincerely,IRA! Mel Gray, Chief Projects Branch 2 Division of Reactor Projects Docket No. 50-286 License No. DPR-26 Inspection Report No. 05000286/2010004 wi
license No. DPR-26 Inspection Report No. 05000247/2010004 wI


===Attachment:===
===Attachment:===
Supplemental Information W. Dean, RA (R10RA Mail) G. Miller, RI D. Hochmuth. DRP M. Dapas, ORA (R10RA Mail) M. Gray, D. Bearde, DRS D. Lew, DRP (R1DRP Mail) B. Bickett, RidsNrrPMlndianPoint J. Clifford, DRP (R1DRP Mail) S. McCarver, Resource D. Roberts, DRS (R1 DRS Mail) P. Cataldo. RidsNrrDorlLpl1-1 Resource P. Wilson, DRS (R1 DRS Mail) M. Halter. RI SUNSI Review Complete: __.::8:,:8=---__(Reviewer's Initials) DOCUMENT NAME: G:\DRP\BRANCH2\a -Indian Point 3\1nspection Reports\2010\2010-004\IP3 2010.004. final.docx After declaring this document "An Official Agency Record" it will be released to the Public. To receive a copy of this document, indicate in the box: "C"::: Copy without !attachment/enclosure "E"::: Copy with attachment/enclosure "N" =No copy ML 103120352 PCataldo/bb for 11102/10 11/02/10 OFFICIAL RECORD COpy Docket No.: License No.: Report No.: Licensee: Facility: Location: Dates: Inspectors: Approved By: U.S. NUCLEAR REGULATORY REGION 05000286/2010004 Entergy Nuclear Northeast Indian Point Nuclear Generating Unit 450 Broadway. Buchanan, NY July 1, 2010 through September 30, P. Cataldo, Senior Resident Inspector -Indian Point M. Halter, Resident Inspector -Indian Point J. Kulp, Senior Resident Inspector -Oyster Creek H. Gray, Senior Reactor Inspector -Region S. McCarver, Project Engineer -Region Mel Gray, Projects Branch Division of Reactor Enclosure TABLE OF
Supplemental Information Distribution (via W.Dean, RA R. Conte, DRS M. Catts, M. Dapas. D. Holody, ORA ) A. Ayegbusi, RI D. Lew. G. Miller, RI OEDO D. Hochmuth, DRP J. Clifford.
 
DRP M. Gray. D. Bearde, DRS D. Collins, B. Bickett, DRP RidsNrrPMlndianPoint Resource D. Roberts. S. McCarver.
 
DRP RidsNrrDorlLpl1-1 Resource P. Wilson. M. Jennerich, DRP ROPreport Resource@nrc.gov SUNSI Review Complete:
bb (Reviewers Initials)
ML 103140355 DOCUMENT NAME: G:\DRP\BRANCH2\a  
-Indian Point 2\1nspection Reports\lP2 IR 201 0-004\IP2 201 0.004.final.docx After declaring this document "An OffICial Agency Record" it will be released to the Public. To receive a copy of this document, indicate in the box: "C" =Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RIIDRP Ilhp RI/DRP I RIIORA NAME MCatts/mc BBickettlbb DHolody/mmm DATE 10125/10 10/25/10 OFFICE RIIDRS I RIIDRP I RIIDRP NAME RConte/rc MGray/mQ DATE 10126/10 11/03/10 OFFICIAL RECORO COpy ,.
Docket No.: License No.: Report No.: Licensee:
Facility:
Location:
Dates: Inspectors:
Approved By: U.S. Nuclear Regulatory Region Entergy Nuclear Northeast Indian Point Nuclear Generating Unit Buchanan, NY July 1, 2010 through September M. Catts, Senior Resident Inspector  
-Unit O. Ayegbusi, Resident Inspector  
-Unit B. Bickett, Senior Project Engineer -Region H. Gray, Senior Reactor Inspector  
-Region J. Nicholson, Health Physicist
-Region Mel Gray, Projects Branch Division of Reactor Enclosure 2


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
...............................................................................................................
IR 05000247/2010004; 7/01/2010
-9/30/2010;
Indian Point Nuclear Generating (Indian Point) Unit 2; Post-Maintenance Testing. This report covered a three-month period of inspection by resident and region-based inspectors.
 
One non-cited violation (NCV) of very low significance (Green) was identified.
 
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process." The cross-cutting aspect for the finding was determined using IMC 0310, "Components within the Cross-Cutting Areas." Findings for which the significance determination process does not apply may be Green, or be assigned a severity level after NRC management review. The NRC's program for overseeing safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
 
===Cornerstone: Mitigating===
 
Systems
: '''Green.'''
A self-revealing NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures and Drawings," was identified because Entergy personnel did not adequately implement the preventive maintenance (PM) procedure for the B reactor trip breaker (RTB}.Specifically, on March 10,2009, Entergy staff did not adequately implement PM Procedure 0-BRK-401-ELC, 'Westinghouse, Reactor Trip and Bypass Circuit Breaker (DB-50)," which resulted in the inoperability of the B RTB shunt trip device function on July 5, 2010. Entergy personnel took immediate corrective actions to replace the B RTB and its associated fuse block assembly.
 
This issue was entered into Entergy's corrective action program as condition report (CR)-IP2-201 0-4451. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems cornerstone and affects the cornerstone objective of ensuring the availability and reliability of systems that respond to initiating events to prevent undesirable consequences (Le. core damage). Specifically, inadequate preventive maintenance contributed to the failure of the shunt trip device function of the B RTB. Using IMC 0609.04, "Phase 1 -Initial Screening and Characterization of Findings," the finding was determined to have very low safety Significance (Green) because the finding did not result in a loss of system safety function because the undervoltage coil was operable; there was not an actual loss of safety function of a single train for greater than its technical speCification allowed outage time; and the issue was not potentially risk significant due to a seismic, flooding, or severe weather initiating event. The finding has a cross-cutting aspect in the area of problem identification and resolution associated with the corrective action program attribute of complete and accurate identification of issues. Specifically, Entergy staff performing preventive maintenance did not identify and communicate RTB conditions completely and accurately such that the B RTB conditions were fully identified in the CAP. [P.1(a) per IMC 0310] (Section 1R19)
 
4


=REPORT DETAILS=
=REPORT DETAILS=
Summary of Plant Status Indian Point Unit 2 began the inspection period operating at full reactor power (100%). The Unit 2 reactor automatically tripped during a planned shutdown on September 3,2010, due to high water level in the 23 steam generator.
Unit 2 remained shutdown for a planned maintenance outage to repair the 21 reactor coolant pump (RCP) motor. Operators returned the plant to full power on September 15, 2010. Unit 2 remained at or near full power for the remainder of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
..................................................................................................................
Cornerstones:
{{a|1R01}}
Initiating Events, Mitigating Systems, and Barrier Integrity 1 R01 Adverse Weather Protection (71111.01 -1 sample) Impending Adverse Weather
==1R01 Adverse Weather Protection ..........................................................................................1R04 Equipment Alignment ....................................................................................................1R05 Fire Protection ...............................................................................................................1R07 Heat Sink Performance .................................................................................................1R11 Licensed Operator Requalification Program .................................................................. 1R12 Maintenance Effectiveness ............................................................................................ 1R13 Maintenance Risk Assessments and Emergent Work Control ....................................... 1R15 Operability Evaluations ................................................................................................ 1R18 Plant Modifications ...................................................................................................... 1R19 Post-Maintenance Testing ........................................................................................... 1R20 Refueling and Outage Activities .................................................................................. 1R22 Surveillance Testing==
 
====a. Inspection Scope====
Because severe weather was forecast in the vicinity of the facility for July 14, 2010, the Inspectors reviewed Entergy's overall preparations/protection for the expected weather conditions.
 
The inspectors walked down systems required for normal operation and shutdown conditions because their safety related functions could be affected, or required, as a result of high wind impacts or the loss of offsite power. The inspectors evaluated the plant staff's preparations in accordance with site procedures to determine if actions were adequate.
 
During the inspection, the inspectors focused on plant specific design features and station procedures used to respond to adverse weather conditions.
 
The inspectors also toured the site to identify loose debris that could become projectiles during a tornado. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant. Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for the systems selected for inspection, and reviewed whether operator actions were appropriate as specified by plant specific procedures.
 
The inspectors also reviewed a sample of corrective action program (CAP) items to verify that the licensee identified adverse weather impact issues at an appropriate threshold and dispositioned them through the CAP in accordance with station corrective action procedures.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one sample as defined in Inspection Procedure 71111.01.
 
====b. Findings====
No findings were identified.
 
===.1 1 Equipment===
 
Alignment Partial System Walkdowns (71111.04Q -3 samples)
 
====a. Inspection Scope====
The inspectors performed partial system walkdowns of the follOwing risk significant systems: July 27,2010,22 safety injection train after post maintenance testing (PMT); September 14, 2010, 22 residual heat removal train after a maintenance outage; and September 27,2010,22 auxiliary feedwater (AFW) pump after a maintenance outage. The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected.
 
The inspectors focused on those conditions that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, technical specification requirements, technical specifications (TSs), work orders (WOs), condition reports (CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions.
 
The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.
 
The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies.
 
The inspectors also reviewed whether Entergy staff had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of three partial system walkdown samples as defined in NRC Inspection Procedure 71111.04.
 
====b. Findings====
No findings were identified . . Full System Walkdown (71111.04S -1 sample)
 
====a. Inspection Scope====
On September 21 and 22, 2010, the inspectors perfonmed a complete system alignment inspection of the safety injection system to verify the functional capability of the system. The inspectors selected this system because it was considered both safety significant and risk significant in the licensee's probabilistic risk assessment.
 
The inspectors inspected the system to review mechanical and electrical equipment line ups, electrical power availability, component lubrication and equipment cooling, hanger and support Enclosure
 
===.1 functionality, operability===
 
of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation.
 
In addition, the inspectors reviewed the CAP database to ensure that system adverse conditions were being identified and appropriately resolved.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one complete system walkdown sample as defined in NRC Inspection Procedure 71111.04.
 
====b. Findings====
No findings were identified.
 
1 R05 Fire Protection Resident Inspector Quarterly Walkdowns (71111.05Q -5 samples)
 
====a. Inspection Scope====
The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition offirefighting equipment in the following risk significant plant areas:
* Pre-Fire Plan (PFP) 160A;
* PFP-205;
* PFP-208;
* PFP-209; and
* PFP-259. The inspectors reviewed areas to assess if Entergy personnel implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the station's fire plan. The inspectors selected fire areas based on their overall contribution to intemal fire risk and their potential to affect equipment that could initiate or mitigate a plant transient.
 
Using the documents listed in the attachment, the inspectors reviewed whether fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.
 
The inspectors also reviewed whether issues identified during the inspection were entered into the licensee's CAP. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of five quarterly fire protection inspection samples as defined in NRC Inspection Procedure 71111.05.
 
====b. Findings====
No findings were identified . . 2 Annual Fire Drill (71111.05A
-1 sample)
 
====a. Inspection Scope====
On August 11, 2010, the inspectors observed a fire brigade activation involving a simulated fire in the vicinity of the hydrazine cylinders, which is located in the turbine building.
 
The observation involved an evaluation of the readiness of the plant fire brigade to fight fires. The inspectors reviewed whether Entergy staff identified performance deficiencies; openly discussed them in a critical manner at the drill debrief; and identified appropriate corrective actions. Specific attributes evaluated by the inspectors were (1) proper wearing of turnout gear and self contained breathing apparatus; (2) proper use and layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader communications, command, and control; (6) search for victims and propagation of the fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one annual fire protection inspection sample as defined in NRC Inspection Procedure 71111.05.<
 
====b. Findings====
No findings were identified.
 
1 R06 Flood Protection Measures (71111.06 -1 sample) Intemal Flooding Review
 
====a. Inspection Scope====
The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; and reviewed the CAP to determine if the licensee identified and corrected flooding problems, and to verify whether operator actions for coping with flooding are adequate.
 
The inspectors also focused on the component cooling water pump room areas to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one internal flood protection measures inspection sample as defined in NRC Inspection Procedure 71111.06.
 
====b. Findings====
No findings were identified.
 
1Licensed Operator Requalification Program (71111.11 Q -1 sample) Quarterly Review
 
====a. Inspection Scope====
On September 1, 2010, the inspectors observed a crew of licensed operators, responding to a simulated event involving a steam generator tube rupture coincident with a loss of offsite power and the failure of select components to automatically start as required.
 
The inspectors observed the scenario in the plant's simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and that training was being conducted in accordance with licensee procedures.
 
The inspectors evaluated the following areas regarding crew and operator performance: Clarity and formality of communications; Implementation of timely actions; Prioritization, evaluation, and verification of annunciator alarms; Usage and implementation of abnormal and emergency procedures; Control board operations; . Identification and implementation of TS actions and emergency plan actions and notifications; and Oversight and direction from control room supervisors.
 
The inspectors compared the crew's performance in these areas to critical task completion reqUirements.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one quarterly licensed operator requalification program sample as defined in NRC Inspection Procedure 71111.11.
 
====b. Findings====
No findings were identified. 1 R Maintenance Effectiveness (71111.12Q -1 sample)
 
====a. Inspection Scope====
The inspectors reviewed the 22 static inverter to assess the effectiveness of maintenance activities on system performance and reliability.
 
The inspectors reviewed, when applicable, system health reports, corrective action program documents, maintenance work orders, and maintenance rule basis documents to ensure performance problems were being identified and properly evaluated within the scope of the maintenance rule. For each sample selected, the inspectors reviewed whether the Enclosure structure, system, and component (SSG) was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and reviewed whether the (a)(2) performance criteria established by Entergy staff was reasonable.
 
For SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2). Additionally, the inspectors determined if Entergy staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one quarterly maintenance effectiveness sample as defined in NRC Inspection Procedure 71111.12.
 
====b. Findings====
No findings were identified.
 
1 Maintenance Risk Assessments and Emergent Work Control (71111.13
-5 samples)
 
====a. Inspection Scope====
The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities affecting risk significant and safety related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work: July 19,2010, elevated risk due to severe weather with 22 fuel oil transfer pump out of service for planned testing; and 22 charging pump, 22 instrument air dryer, and feeder 96951 out of service for emergent maintenance; July 28,2010, elevated risk due to 23 charging pump out of service for planned maintenance and 6.9kV relay functional testing; August 19, 2010, elevated risk for 480 volt degraded voltage function and emergency diesel generator (EDG) out of service for planned calibration and testing of 480 volt undervoltage alarms; August, 24, 2010, elevated risk for 21 AFW pump test, and alternate safe shutdown supply breaker to 21 AFW pump test, during emergent maintenance on individual rod position indication D-8; and September 16,2010, elevated risk due to 21 EDG, refueling water storage tank level indicator, and residual heat removal valve 884 out of service for planned maintenance; and 21 service water pump out of service for emergent maintenance.
 
The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones.
 
As applicable for each activity, the inspectors verified that Entergy personnel performed risk assessments as required by 10 CFR 50.65{a)(4)and that the assessments were accurate and complete.
 
When Entergy personnel performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the station's probabilistic risk analyst or shift technical advisor, to verify plant conditions were consistent with the risk Enclosure assessment.
 
The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of five maintenance risk and emergent work control inspection sample as defined in NRC Inspection Procedure 71111.13.
 
====b. Findings====
No findings were identified.
 
1 R15 Operability Evaluations (71111.15 3 samples)
 
====a. Inspection Scope====
The inspectors reviewed the following issues:
* July, 6, 2010, 480 volt switchgear room high temperature alarm;
* July 20, 2010, EDG starting air capacity; and
* August 17, 2010, EDG fuel oil leaks. The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred.
 
The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to Entergy's evaluations to determine whether the components or systems were operable.
 
Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled.
 
The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.
 
Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of three operability evaluations inspection samples as defined in NRC Inspection Procedure 71111.15.
 
====b. Findings====
No findings were identified.
 
1 R Plant Modifications (71111
 
===.18 -1 sample) Temporary===
 
Modifications
 
====a. Inspection Scope====
The inspectors reviewed the following temporary modification to verify that the safety functions of affected safety systems were not degraded:
On July 28, 2010, Entergy staff implemented Engineering Change (EC) 23681 in response to high upper thrust bearing temperatures on the 21 RCP motor. The temporary modification raised the upper thrust bearing temperature alarm setpoint from 185F to 190F and the. manual trip setpoint from 200F to 205F. This temporary modification remained in place until repair of the 21 RCP motor was completed September 13, 2010. The inspectors reviewed the temporary modification and the associated safety evaluation screening against the system design bases documentation, including the UFSAR and the TSs, and verified that the modification did not adversely affect the system operability/availability.
 
The inspectors also reviewed whether the installation and restoration were consistent with the modification documents and that configuration control was adequate.
 
Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and Entergy personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one sample for temporary plant modifications as defined in NRC Inspection Procedure 71111.18.
 
====b. Findings====
No findings were identified. 1 R Post Maintenance Testing (PMT) (71111.19
-7 samples)
 
====a. Inspection Scope====
The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability: . July 5,2010, B reactor trip breaker (RTB) replacement; July 6, 2010, temperature average signal computer after summing amplifier repair; July 21,2010,22 charging pump after internal valve replacement; July 21, 2010, rod position indicators E13 and L 13 after replacement; August 25, 2010, pilot operated relief valve disconnect switches EDC 10 and 11 after maintenance; September 7, 2010, 22 steam generator level bistable LC 427 NB after replacement; and September 16, 2010, 21 EDG after maintenance outage. The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities to determine (as applicable)the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; and that test instrumentation was appropriate.
 
The inspectors evaluated the activities against the TSs, the UFSAR, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements.
 
In addition, the inspectors reviewed corrective action documents associated with PMTs to determine whether Entergy personnel were identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of seven PMT inspection samples as defined in NRC Inspection Procedure 71111.19.
 
====b. Findings====
Reactor Trip Breaker (RTB) Preventative Maintenance Procedure was not Adequately Implemented
 
=====Introduction:=====
A self-revealing Green NCV of 10 CFR 50, Appendix B, Criterion V "Instructions, Procedures and Drawings," was identified because Entergy staff did not adequately implement the PM procedure for the B RTB in March 2009.
 
=====Description:=====
On July 5,2010, control room operators observed the B RTB red indicating breaker closed lights were extinguished.
 
The red indicating breaker closed lights are in series with the shunt trip device and provide indication in the control room that the breaker trip mechanism is functioning properly.
 
After troubleshooting was conducted, Entergy operators determined the shunt trip device function was inoperable, entered the applicable TS action statement TS 3.3.1, "Reactor Protection System (RPS) Instrumentation," and issued CR-IP2-2010-4451.
 
The associated bypass breaker was racked in and the B RTB and its associated fuse block were replaced.
 
The B RTB shunt trip device was restored to operability in the timeframe provided in the TS action statement.
 
Entergy personnel generated was to replace fuse block assemblies for the remaining reactor trip and bypass breakers at the site. Indian Point Unit 2 has two reactor trip breakers in service that are normally closed during normal plant operations and two bypass breakers in parallel to each RTB for performing PM. The breakers have two tripping mechanisms which include the undervoltage coil and the shunt trip device. The tripping mechanisms serve to open the RTB when the RPS automatic trip logic is made up to interrupt power to the control rod drive mechanisms, which allows the shutdown and control rods to fall into the core by Enclosure i
gravity. The shunt trip device serves a redundant function that ensures the breaker opens if the undervoltage coil failed to function properly.
 
Entergy personnel performed an apparent cause evaluation (ACE) of the B RTB failure and determined that the B RTB red indicating lights in the control room were extinguished due to a degraded control power fuse holder. This degradation included a broken corner of the insulating material, loose fuse clips, exposed copper due to worn silver coating on contact points, distorted fuse Clip blades and poor contact resistance checks. The fuse holder when installed into the fuse case had insufficient tension and could be easily removed or installed without requiring significant force. Entergy personnel determined the degraded condition was due to a lack of questioning attitude and attention to detail by maintenance personnel during past PM inspections.
 
Entergy's ACE noted that the degraded condition developed over the course of several years and was evident at a minimum during the March 10,2009 performance of PM Procedure 0-BRK-401-ELC "Westinghouse, Reactor Trip and Bypass Circuit Breaker (DB-50)," which includes a step for checking the fuse holder. Entergy's corrective actions included:
reinforce conduct of maintenance in regards to activities of plant equipment within the maintenance and operations departments; enhance guidance for fuse block inspection in PM procedures; and evaluate the need for maintenance and operations department training enhancements associated with fuses and fuse block inspections.
 
The inspectors reviewed the ACE and completed PM procedure, and also identified that maintenance personnel identified issues with the control power fuses and a chip on the fuse holder; however, the adverse conditions were not communicated to the responsible engineer as required by Step 4.2.7 "Notify Responsible Engineer AND Supervisor of unusual conditions AND record below." In addition, a CR was not issued in accordance with the PM procedure and station standards.
 
The inspectors noted that Step 3.10 of the PM procedure states that "All unacceptable components and conditions SHALL be documented on Attachment 1 and Unacceptable Component Tracking Sheet accepted or corrected under the direction of the Component Engineer;" however, the attachment was not completed.
 
The inspectors also identified a separate issue with the procedure where maintenance personnel did not perform cell switch inspection and lubrication as required by Step 4.2.9. This step is necessary to ensure that the cell switches reset to their shelf position upon removal of a RTB and the reactor protection circuitry is established as designed.
 
Entergy personnel documented this issue in CR-IP2-201 0-5317 and performed Step 4.2.9 of the procedure during a forced outage in September 2010 under WO 249229 and did not identify an adverse condition.
 
Entergy's corrective actions included reviewing a sample of work packages under CR-IP3-201 0-1 022 to ensure all work packages were fully completed.
 
=====Analysis:=====
The performance deficiency associated with this finding was that Entergy personnel did not adequately implement the PM procedure for the B RTB in March 2009. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems cornerstone and affects the cornerstone objective of ensuring the availability and reliability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, an inadequate PM implementation contributed to the failure of the shunt trip device function of the B RTB. Using IMC 0609.04, "Phase 1 -Initial Screening and Characterization of Findings," the finding was determined to have very low safety significance (Green) because the finding Enclosure did not result in a loss of system safety function because the undervoltage coil was operable; there was not an actual loss of safety function of a single train for greater than its technical specification allowed outage time; and the issue was not potentially risk significant due to a seismic, flooding, or severe weather initiating event. The finding has a cross-cutting aspect in the area of problem identification and resolution associated with the corrective action program attribute of complete and accurate identification of issues. Specifically, Entergy staff did not identify and communicate RTB conditions completely and accurately such that the B RTB conditions were fully identified in the CAP. [P.1.(a) per IMC 0310]
 
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures and Drawings," requires, in part, that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances and shall be accomplished in accordance with these procedures.
 
Contrary to the above, on March 10,2009, maintenance personnel did not adequately implement PM Procedure 0-BRK-401-ELC "Westinghouse, Reactor Trip and Bypass Circuit Breaker (DB-50)" which resulted in the inoperability of the B RTB shunt trip device on July 5, 2010. Entergy personnel took immediate corrective actions to replace the B RTB and its associated fuse block assembly.
 
Because this violation was of very low safety significance and it was entered into Entergy's CAP as CR-IP2-201 0-4451, this violation is being treated as a NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 500024712010004-01, Reactor Trip Breaker Preventative Maintenance Procedure was not Adequately Implemented. 1 Refueling and Outage Activities (71111.20
-1 sample)
 
====a. Inspection Scope====
The inspectors reviewed the outage safety plan and contingency plans for the Unit 2 planned maintenance outage to repair the 21 RCP, conducted September 3 -15, 2010. The inspectors' review considered whether Entergy personnel appropriately considered risk, industry experience, and previous site performance in developing and implementing a plan that assured maintenance of defense in depth with regards to reactor safety. During the maintenance outage, the inspectors observed portions of the shutdown and cooldown processes and monitored Entergy operator controls over the outage activities listed below: Configuration management, including maintenance of defense in depth, is commensurate with the outage safety plan for key safety functions and compliance with the applicable TSs when taking equipment out of service; Clearance activities, including confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing; Status and configuration of electrical systems to ensure that TSs and outage planning requirements were met, and controls over switchyard activities were appropriate; Monitoring of decay heat removal processes, systems. and components; Controls over activities that could affect reactivity; Maintenance of secondary containment as required by the TS; Enclosure Startup and ascension to full power operation, tracking of startup prerequisites, and walkdown of containment to verify that debris had not been left which could impact emergency core cooling system suction strainers; Station personnel identification and resolution of problems related to maintenance outage activities; and Work hours for fatigue concerns.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one other outage inspection sample as defined in NRC Inspection Procedure 71111.20.
 
====b. Findings====
No findings of significance were identified. Surveillance Testing (71111.22
-4 samples)
 
====a. Inspection Scope====
The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems, and components, to assess whether test results satisfied Technical Specifications, UFSAR, technical requirements manual, and Entergy procedure requirements.
 
The inspectors verified that: test acceptance criteria were sufficiently clear; tests demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had accurate calibrations and appropriate range and accuracy for the application; tests were performed as written; and applicable test prerequisites were satisfied.
 
Following the tests, the inspectors considered Whether the test results supported conclusions that equipment was capable of performing the required safety functions.
 
The following surveillance tests were reviewed: June 30, 2010, 2-PT-Q62, high steam flow and turbine first stage pressure bistables test; July 30,2010, 2-PT-Q088, inservice testing of component cooling water check valves 790, 791. 798 &796. 793; August 4,2010, 2-PT-Q58, steam generator level bistables test; and August 19, 2010, 2-PT-M048, 480V undervoltage alarm test. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of four surveillance testing inspection samples as defined in NRC Inspection Procedure 71111.22.
 
====b. Findings====
No findings were identified.
 
===.1 Cornerstone:===
 
Emergency Preparedness 1 EP6 Drill Evaluation (71114.06
-1 sample) Emergency Preparedness Drill Observation
 
====a. Inspection Scope====
The inspectors evaluated the conduct of a routine Entergy emergency drill on September 1, 2010, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities.
 
The inspectors observed emergency response operations in the simulator to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures.
 
The inspectors also attended the station drill critique to compare inspector observations with those identified by Entergy staff in order to evaluate Entergy's critique and to verify whether the Entergy staff was properly identifying weaknesses and entering them into the CAP. Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one sample as defined in NRC Inspection Procedure 71114.06.
 
====b. Findings====
No findings were identified.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
............................................................................................................... 40A1 Performance Indicator Verification ............................................................................... 40A2 Identification and Resolution of Problems.................................................................... 40A3 Event FOllow-Up .......................................................................................................... 40A6 Meetings ..................................................................................................................... ATTACHMENT:
40A 1 Performance Indicator Verification (71151 -2 samples) Mitigating Systems Performance Index -High Pressure Injection Systems (MS07)
 
====a. Inspection Scope====
The inspectors sampled Entergy submittals for the mitigating systems performance index -high pressure injection systems PI for the period from July 2009 through June 2010. To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute (NEt) Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed Entergy's operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.
 
The inspectors also reviewed Entergy's issue report database to determine if problems had been identified with the PI data collected or transmitted for this indicator and none were identified.
 
Specific documents reviewed are described in the attachment to this report. These activities constitute completion of one mitigating systems performance index -high pressure injection system sample as defined in NRC Inspection Procedure 71151. Enclosure
 
===.1
 
====b. Findings====
No findings were identified . . 2 Mitigating===
 
Systems Performance Index -Heat Removal System (MS08)
 
====a. Inspection Scope====
The inspectors sampled Entergy submittals for the mitigating systems performance index -heat removal system PI for the period from July 2009 through June 2010. To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports, mitigating systems performance index derivation reports, and NRC integrated inspection reports to validate the accuracy of the submittals.
 
The inspectors also reviewed Entergy's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.
 
Specific documents reviewed are described in the attachment to this report. These activities constitute completion of one mitigating systems performance index -heat removal system sample as defined in NRC Inspection Procedure 71151.
 
====b. Findings====
No findings were identified.
 
40A2 Identification and Resolution of Problems (71152 -2 samples) Routine Review of Problem Identification and Resolution Activities
 
====a. Inspection Scope====
As required by Inspection Procedure 71152, "Identification and Resolution of Problems," the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that issues were being entered into Entergy's CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed.
 
In order to assist with the identification of repetitive equipment failures and specific human performance issues for fOllOW-Up, the inspectors performed a daily screening of items entered into the CAP. The inspectors reviewed attributes that included:
(1) complete and accurate identification of the problem; (2) timely correction, commensurate with the safety significance; (3) evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and (4) classification, prioritization, focus, and timeliness of corrective actions. These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter. Specific documents reviewed during this inspection are listed in the attachment.
 
====b. Findings====
No findings were identified . . 2 Annual Sample -Review of Nonfunctional Emergency Light EL-6
 
====a. Inspection Scope====
The inspectors selected for review 0-5037 to determine if problems were being properly identified, characterized, and entered into the CAP for evaluation and resolution.
 
This documented a failure of Emergency Light (EL) EL-6 due to its light beams being misaligned during the last functional test. Entergy performed an extent of condition review with no issues identified.
 
The inspectors also conducted walkdowns and interviewed plant personnel to verify proper EL alignment.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one in-depth problem identification and resolution sample as defined in NRC Inspection Procedure 71152.
 
====b. Findings and Observations====
No findings were identified.
 
The inspectors identified the issue documented in CR-IP2-2010-5037 during a plant walkdown.
 
The inspectors reviewed the last completed Procedure 2-PT-M49A1B "Appendix R Emergency Lighting," and found that EL-6 had electrolyte added to its internal battery. Access to the battery is through the top cover, where the light beams are attached, and manipulating the top cover easily moves the light beams out of position.
 
The inspectors determined that the procedure checks the alignment of the light beams before adding electrolyte to the battery, but does not verify the light beams are in the correct position once the cover and lights are re-instal/ed.
 
This issue was entered into the licensee's CAP as CR-IP3-201 0-2576. The inspectors determined this issue is minor because the light found out of position was only used for access and egress paths; operations personnel carry flashlights when responding to fires; there was no impact on the operation of a safety related component; and no other light beams were found out of position over the last year. The inspectors determined that Entergy's corrective action to revise the functional test procedure to verify light beam alignment upon completion of the procedure is adequate . . 3 Annual Sample -Buried Pipe Inspection and Monitoring Program
 
====a. Inspection Scope====
The inspectors interviewed the Program Owner (Responsible Engineer)for the Indian Point Buried Pipe Inspection and Monitoring Program and reviewed the related applicable procedures for the program. The inspectors used as a reference the Electric Power Research Institute (EPRI) and NEI guidelines for buried pipe systems. Field observations were made of the areas of past and current buried pipe activities.
 
These included the Unit 2 and Unit 3 condensate storage tank (CST) and auxiliary feedwater
 
===.1 19 (AFW) piping, and the piping exiting the Unit 3 reactor water storage tank to under the independent===
 
spent fuel storage installation (ISFSI) haul path. The inspection scope included determining the status of site activities and plans to monitor and inspect buried piping and storage tanks. The inspectors ensured these activities met or exceeded the EPRI and NEI guidance and requirements to understand the condition of these components to minimize the occurrence of leakage. SpeCific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one in-depth problem identification and resolution sample, as defined in NRC Inspection Procedure 71152.
 
====b. Findings and Observations====
No findings were identified.
 
A leak in the Unit 2 AFW system 8-inch diameter return line to the CST was identified by Entergy staff on February 15,2009 and repaired.
 
In September 2009, guided wave inspection conducted by station personnel identified Level 2 G-scan indications in both the Unit 2 and Unit 3 AFW CST 12-inch diameter suction lines. Level 2 G-scan indications are areas of moderate interest where follow-up is recommended.
 
Entergy entered this condition for evaluation into the CAP as CR-IP2-2009-00666.
 
40A3 Event Follow-up (71153 -3 samples) (Closed) Licensee Event Report 05000247/2010-004-00, Plant Operation Outside Technical Specifications Due to a Leak in the Reactor Coolant Pressure Boundary.
 
====a. Inspection Scope====
On March 18, 2010, while Indian Point Unit 2 was shutdown for a refueling outage, Entergy staff identified boron accumulation at a socket weld from the reactor coolant pressure boundary on a three-quarter inch line located upstream of check valve 256B associated with 22 RCP seal bypass line. Based on visual inspections conducted by Entergy staff during its boric-acid walkdowns, Entergy personnel concluded that the leak most likely existed during plant operation based on the amount of dry boron accumUlation at the weld defect area. Entergy engineering personnel characterized the flaw as a rounded weld defect in the socket weld, which likely was introduced at the time of system construction and which propagated through-wall over time during plant operations as the result of service induced loading conditions.
 
Entergy maintenance technicians repaired the defect during the April 2010 outage. Entergy staff determined the leakage could have existed during plant operation and, therefore, the plant could have been operating contrary to TS 3.4.13, "RCS Operational Leakage," which limits operational pressure boundary leakage to zero. The inspectors reviewed the Licensee Event Report (LER), Entergy's evaluation of the event, and associated corrective actions contained in CR-I P2-20 1 0-01631. The inspectors determined that the weld defect and resultant leakage was not within Entergy's ability to foresee and correct based on review of Entergy's visual examination results, corrective action reviews and associated non-destructive examination requirements for this weld. This review was supplemented by inspector observations of this prior leakage condition observed by inspectors during the outage as part of NRC Inspection Procedure 71111.08.
 
Specifically, the inspectors affirmed that there were no in-service inspection requirements not implemented or previous corrective action information available to Entergy personnel that would have detected or reasonably indicated a weld defect for this particular socket weld. The inspectors also affirmed Entergy staff identified the leakage at the first reasonable opportunity.
 
Therefore, the inspectors concluded operation of Indian Point Unit 2 with RCS pressure boundary leakage is prohibited by TS 3.4.13. However, the inspectors determined that this weld defect could not have been avoided or detected by Entergy's quality assurance program or other related control measures, and did not constitute a performance deficiency.
 
These activities constitute completion of one event follow-up sample as defined in NRC Inspection Procedure 71153.
 
====b. Findings====
This issue is considered within the traditional enforcement process because there was no performance deficiency identified and NRC IMC 0612, Appendix B, "Issue Screening" directs disposition of this issue in accordance with the NRC Enforcement Policy. The inspectors used the Enforcement Policy, Section 6.1 -Reactor Operations, to evaluate the significance of this violation.
 
The inspectors concluded that the violation is more than minor and best characterized as Severity Level IV (very low safety Significance)because it is similar to Enforcement Policy Section 6.1, Example d.1. Additionally, the inspectors assessed the risk associated with the issue by using IMC 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations." The inspectors screened the issue and determined that RCS leakage is considered a Loss-of-Coolant Accident initiator, and evaluated using the Initiating Event criteria in Appendix A. Based on the weld defect size and characterization of the flaw, it is not expected this existing flaw would have impacted the structural integrity of the bypass line, the leakage would not result in exceeding the TS limit for identified RCS leakage (10 gpm) nor would the leakage have likely affected other mitigation systems resulting in a total loss of their safety function.
 
As a result, this issue would screen as very low safety significance (Green). Because this issue is of very low safety significance (Green) and it has been determined that this issue was not within Entergy's ability to foresee and correct, that Entergy staff's actions did not contribute to the degraded condition, and that actions taken were reasonable to identify and address this matter, and as such no performance deficiency exists, the NRC has decided to exercise enforcement discretion in accordance with Section 3.5 of the NRC Enforcement Policy and refrain from issuing enforcement action for the violation of TSs (EA-1 0-212). Further, because licensee actions did not contribute to this violation, it will not be considered in the assessment process or the NRC's Action Matrix. This LER is closed. Specific documents reviewed during this inspection are listed in the attachment.
 
===.2 Loaded Multi-Purpose===
 
Canister Stuck During Transfer from the HI-TRAC Transfer Cask to a H I-STORM Storage Cask
 
====a. Inspection Scope====
The inspectors reviewed the below listed equipment issue for plant status and mitigating actions to evaluate Entergy staff performance and confirm that Entergy staff implemented actions and notifications (if required)in accordance with station procedures.
 
From July through September, 2010, Entergy personnel conducted a campaign to place selected spent fuel elements into dry cask storage. On August 11, 2010, during the transfer of a fully loaded Multipurpose Canister (MPC) MPC-32 canister from the HI-TRAC transfer cask into a HI-STORM storage cask, the MPC became lodged while partially inserted into the HI-STORM cask. The MPC had been lowered approximately 18 inches into the H I-STORM from the H 1-TRAC, but became lodged and could not be lowered or raised with the fuel storage building (FSB) gantry crane. Through consultation with representatives of Holtec International (Holtec), the storage system vendor, Entergy personnel determined the problem to be a result of a mis-alignment of the HI-TRAC, the HI-STORM, and the mating device that joins the HI-TRAC to the HI-STORM for the MPC transfer.
 
After connections to the mating device and HI-TRAC were loosened, the FSB gantry crane main hOist was used to take up some of the HI-TRAC load. This manipulation freed up the MPC and it was able to be raised back into the HI-TRAC. The HI-TRAC and MPC were then lifted off the HI-STORM and mating device and placed into a safe storage position on August 13, 2010. Entergy personnel subsequently resumed dry cask operation during the week of August 16, 2010 and the MPC was able to be loaded into the HI-STORM on August 19.2010. The HI-STORM was subsequently placed on the ISFSI pad and no additional problems were encountered.
 
The inspectors reviewed Entergy actions and decision making to verify decisions were consistent with a conservative approach to assessing and addressing the condition.
 
The inspectors reviewed whether Entergy evaluations (and/or vendor supplied correspondence)were supported and addressed the thermal and structural performance of the MPC including a focus on the heat load of this loaded MPC to ensure the heat load remained below the Final Safety Analysis Report (FSAR) maximum permissible heat load limits. The inspectors also reviewed station evaluations that concluded that there was no structural damage to the air channels inside the HI-STORM and the thermal performance of the MPC and HI-STORM was not adversely affected.
 
These activities constitute completion of bne event follow-up sample as defined in NRC Inspection Procedure 71153.
 
====b. Findings====
No findings were identified.
 
The inspectors determined that Entergy and vendor-supplied evaluations appropriately concluded that the MPC was not adversely impacted in either thermal or structural performance.
 
Entergy entered the issue into the CAP and revised Holtec procedure 2-DCS-009-GEN, "MPC Transfer & HI-STORM Movement," to ensure that the mating device is properly aligned with the HI-STORM . . 3 Automatic Reactor Trip on High Steam Generator Water Level a. Inspection Scoge The inspectors reviewed the below listed event for plant status and mitigating actions to evaluate Entergy performance and confirm that Entergy operators implemented actions and notifications (if required)in accordance with station procedures.
 
The inspectors evaluated the response of control room personnel following the automatic reactor trip that occurred on September 3,2010, during a normal shutdown for a planned maintenance outage for repairs to the 21 reactor coolant pump motor. The Indian Point Unit 2 reactor automatically tripped from approximately 41% power in response to a main generator trip caused by high water level in the 23 steam generator.
 
The inspectors reviewed plant computer data, including the sequence of events report, evaluated plant parameter traces, and discussed the event with plant personnel, to verify that plant equipment responded as expected.
 
and to ensure that operating procedures were appropriately implemented.
 
The inspectors verified that operations personnel took appropriate actions in accordance with procedures in response to control rod H-8 indicating that the rod did not fully insert. The inspectors also verified that Entergy's post-trip review group (PTRG) identified the most probable cause(s) of the trip to facilitate corrective actions prior to restart. This event and the PTRG report were entered into Entergy's corrective action program as CR-IP2-2010-5484.
 
Specific documents reviewed during this inspection are listed in the attachment.
 
These activities constitute completion of one event follow-up sample as defined in Inspection Procedure 71153.
 
====b. Findings====
No findings of Significance were identified.


=SUPPLEMENTAL INFORMATION=
The inspectors determined that operational response to the reactor trip was appropriate and that the indication problem with control rod H-8 was verified and corrected.
 
The inspectors will conduct further review of the root cause evaluation (RCE) and associated corrective actions in conjunction with review of the licensee event report to be submitted by Entergy personnel.
 
40A6 Meetings, Including Exit Exit Meeting Summary On October 28, 2010, the inspectors presented the inspection results of the integrated inspection to Mr. Joseph Pollock, Site Vice President, and other members of the Entergy staff. The licensee acknowledged the conclusions and observations presented.
 
The inspectors asked whether any materials examined during the inspection should be considered proprietary.
 
No proprietary information was identified.
 
ATTACHMENT:
 
=SUPPLEMENTAL
INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
........................................................................................................
Entergy Personnel
==LIST OF ITEMS==
J. Pollock Site Vice President
OPENED, CLOSED AND DISCUSSED .............................................................
: [[contact::R. Allen NDE Level III]], Code Programs H. Anderson Specialist
==LIST OF DOCUMENTS REVIEWED==
-Nuclear Safety/Licensing
............................................................................................ LIST OF ACRONyMS .................................................................................................................. Enclosure 
N.Azevedo
: SUMMARY OF FINDINGS
Supervisor
: IR 05000286/2010004; 7/1/10 -9/30/10; Indian Point Nuclear Generating (Indian POint) Unit 3; Maintenance Effectiveness. This report covered a three-month period of inspection by resident and region based inspectors. One finding of very low significance (Green) was identified. This finding was also determined to be a non-cited violation (NCV) of NRC requirements. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process." The cross-cutting aspect for the finding was determined using
-Engineering
: IMC 0310, "Components within the Cross-Cutting Areas." Findings for which the significance determination process (SDP) does not apply may be Green, or be assigned a severity level after NRC management review. The NRC's program for overseeing safe operation of commercial nuclear power reactors is described in
J. Baker Shift Manager M. Burney Specialist
: NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. Cornerstone: Mitigating Systems Green: A self-revealing, non-cited violation (NCV) of very low safety Significance (Green) of 10
-Nuclear Safety/Licensing
: CFR 50, Appendix B, Criterion XVI, "Corrective Actions," was identified because Entergy personnel did not adequately identify and correct a condition adverse to quality to ensure the continued availability of the safety related 31 static inverter. Specifically, Entergy personnel did not complete previously-identified corrective actions to ensure capacitors in critical components of the inverter were identified and replaced in a timely manner prior to the occurrence of age-related failures. Entergy personnel determined that degraded commutation capacitors were the cause of a fuse failure on September 14, 2010, and were identified to be 13 years old and installed significantly longer than the nine years recommended by the vendor. Entergy personnel entered the issue into the corrective action program and replaced the capacitor. The finding was more than minor because the finding was associated with the Mitigating Systems cornerstone attribute of eqUipment performance and affected the cornerstone objective of ensuring the availability and reliabifity of systems that respond to initiating events to prevent undesirable consequences. Specifically, the 31 static inverter incurred unnecessary unavailability hours and was inoperable and unavailable for approximately five days following the fuse failure on September 14, 2010. The inspectors determined the finding was of very low safety significance (Green) because the finding was not a design or qualification deficiency, did not represent a loss of system safety function, and was not risk significant with respect to external events. The inspectors determined that this finding had a cross-cutting aspect in the area of Problem Identification and Resolution because Entergy personnel did not complete adequate and timely corrective actions to implement a capacitor program and identify critical capacitors for replacement prior to a failure that resulted in the unavailability of a safety related inverter. [P.1(d) per
R. Burroni Manager -System Engineering
: IMC 0310] (Section 1 R12) Enclosure 
T. Cole Project Manager -NUC G. Dahl SpeCialist -Nuclear Safety/licensing
: REPORT DETAILS Summary of Plant Status Indian Point Unit 3 began the inspection period operating at full reactor power (1000/0). On September 9, 2010, operators manually tripped the reactor after a service water leak was observed inside the main generator exciter cabinet. Repairs were performed and the operators returned Unit 3 to full power on September 17, 2010. Unit 3 remained at or near full power during the remainder of the inspection period. 1. REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 'I R01 Adverse Weather Protection (71111.01 --1 sample) Severe Thunderstorm Warning Preparedness a. Inspection Scope Using procedure
R. Daley Engineer III -Nuclear G. Dean Shift Manager D. Dewey Shift Manager G. Hocking Supervisor
: OAP-008, "Severe Weather Preparations," the inspectors reviewed Entergy's preparations for impending thunderstorms on July 19,2010, which coincided with the notification of a National Weather Service severe thunderstorm warning. The inspectors also reviewed 3-S0P-EL-005, "Operation of On-Site Power Sources," to evaluate any additional actions, including plant risk assessments, as a result of the occurrence of a 345kV grid disturbance that occurred soon after their entry into 008. This inspection represented one inspection sample. b. Findings No findings were identified. 1 R04 Equipment Alignment (71111.04Q --4 samples) Partial System Walkdowns a. Inspection Scope The inspectors performed partial system walkdowns to verify the operability of redundant or diverse trains and components during periods of system train unavailability, and where applicable, following return to service after maintenance. The inspectors reviewed system procedures, the Updated Final Safety Analysis Report (UFSAR), and system drawings to verify that the alignment of the applicable system or component supported its required safety functions. The inspectors also reviewed applicable condition reports or work orders to ensure that Entergy personnel had identified and properly addressed equipment deficiencies that could potentially impair the capability of the available train. The documents reviewed during this inspection are listed in the Attachment. Enclosure The inspectors performed a partial walkdown on the following systems, which represented four inspection samples: 32 containment spray (CS) pump during 31 CS pump test on June 27, 2010; 31 and 33 auxiliary boiler feed pumps (ABFP) during 32 ABFP maintenance on August 2,2010; 32 and 33 emergency diesel generators (EDGs) during 31 EDG maintenance on August 10 -12, 2010; and 31 component cooling water (CCW) train during planned work on 33 CCW pump breaker on August 25, 2010. b. Findings No findings were identified. 1 Fire Protection (71111. 05Q -6 samples) Resident Inspector Quarterly Walkdowns a. Inspection Scope The inspectors conducted tours of selected Unit 3 fire areas to assess the material condition and operational status of applicable fire protection features. The inspectors reviewed, consistent with the applicable administrative procedures, whether: combustible material and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with Entergy's fire protection program. The inspectors also evaluated the fire protection program for conformance with the requirements of License Condition 2.K. The documents reviewed during this inspection are listed in the Attachment. PFP (Pre-Fire Plan) 351A;
-Radiation
: PFP 355;
Protection
: PFP 356;
R. Lee Buried Pipe and Tank Program Lead Engineer J. Lijoi Superintendent
: PFP 383;
-I&C L Lubrano Senior Lead Engineer R. Mages Senior HPfChemical
: PFP 384; and Radiological and Environmental Services room battery failure on September 14, 2010. b. Findings No findings were identified. Enclosure 
Specialist
: R07 Heat Sink Performance (71111.07 -1 sample) a. Inspection Scope The inspectors evaluated maintenance activities and reviewed inspection data associated with the 31 EDG jacket water and lube oil heat exchangers on August 10, 2010. The inspectors reviewed applicable design basis information and commitments associated with Entergy's Generic Letter 89-13 program to validate that maintenance activities were adequate to ensure the system could perform its required safety function. The inspectors reviewed radiographic results for selected piping segments to ensure pipe corrosion and conditions adverse to quality were being identified and corrected. This inspection represented one sample for heat sink performance. b. Findings No findings were identified. 1R11 Licensed Operator Regualification Program (71111.11 Q -1 sample) Quarterly Review a. Inspection Scope On August 10, 2010, the inspectors observed a licensed operator requalification training evaluation conducted in the plant-reference simulator, to verify appropriate operator performance, and that evaluators identified and documented crew performance problems, as applicable. The inspectors evaluated the performance of risk significant operator actions, including the use of emergency operation procedures. The inspectors assessed the clarity and the effectiveness of communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operations, and the oversight and direction provided by the control room supervisor. The inspectors reviewed simulator fidelity to verify correlation with the actual plant control room, and to verify that differences in fidelity that could potentially impact training effectiveness were either identified or appropriately dispositioned. Licensed operator training was evaluated for conformance with the requirements of 10
T. McCaffrey
: CFR 55, "Operator Licenses.It This observation of licensed-operator evaluations represented one inspection sample. b. Findings No findings were identified. 1R12 Maintenance Effectiveness (71111.12Q -2 samples) a. Inspection Scope The inspectors reviewed performance-based problems that involved selected structures, systems, and components (SSCs) to assess the effectiveness of maintenance activities Enclosure and to verify activities were conducted in accordance with site procedures and 10
Manager -Design Engineering
: CFR 50.65 (The Maintenance Rule). The reviews focused on: Evaluation of Maintenance Rule scoping and performance criteria; Verification that reliability issues were appropriately characterized; Verification of proper system and/or component unavailability; Verification that Maintenance Rule (a)(1) and (a)(2) classifications were appropriate; Verification that system performance parameters were appropriately trended; For 8SGs classified as Maintenance Rule (a)(1). that goals and associated corrective actions were adequate and appropriate for the circumstances; and Identification of common cause failures. The inspectors also reviewed system health reports. maintenance backlogs. and Maintenance Rule basis documents. The documents reviewed during this inspection are listed in the Attachment. The following systems and/or components were reviewed and represented two inspection samples: 138 KV system and breaker BT 5-6 failure on June 18. 2010; and 31 static inverter unavailability on August 24,2010. b. Findings Introduction: A self-revealing, non-cited violation (NCV) of very low safety significance (Green) of 10
: [[contact::T. Orlando Director]], Engineering
: CFR 50, Appendix B. Criterion XVI, "Corrective Actions," was identified because Entergy personnel did not adequately identify and correct a condition adverse to quality to ensure the continued availability of the safety-related 31 static inverter. Specifically, Entergy personnel did not implement previously-identified corrective actions to ensure capacitors in critical components of the inverter were identified and replaced in a timely manner prior to the occurrence of age-related failures. Description: On September 14,2010, the safety-related 31 static inverter performed an automatic swap-over from its safety-related power source to its non-safety related power source due to a fuse failure. This occurrence required Entergy operators to enter a seven-day shutdown limiting condition for operation in accordance with technical specifications. Entergy personnel began troubleshooting actions. which included contracted technical consultation, to determine the cause of the fuse failure in the A4 commutation section of the inverter. Entergy personnel's troubleshooting actions included, for example, visual inspections of solder joints, circuit card connection checks, circuit card operation and revision history (ageihistory). diode checks and voltage profiles, and commutation circuit operational checks. Based on review of troubleshooting test data, commutation capacitors C1 and G2, located in the A4 section, were determined by Entergy personnel to be the cause of the fuse failure. Entergy staff determined these capacitors had been in service for 13 years which is Significantly longer tha'n the nine years recommended by the vendor. These capacitors were replaced and the static inverter was successfully load tested and placed back into normal operation on September 19,2010. Enclosure The inspectors reviewed the corrective action database, which included a similar fuse failure in August 2010 (CR-IP3-2010-02530). and other failures that dated back to 2001. During this review, the inspectors noted that a capacitor improvement program had been previously identified by Entergy staff as a program that was needed due to failures that included age-related causes. For example, Entergy's root cause evaluation (RCE) regarding a 2007 power supply failure associated with a Unit 2 main boiler feedwater pump (CR-IP2-2007-01046) documented the following information: A December 2001 kickoff meeting was held to develop a capacitor program; A 2002 corrective action (CA) to address capacitor aging/replacement was cancelled; Entergy's RCE team noted that from May 2003 to March 2007 there were no further actions taken to address age degradation of electrolytic capacitors and that the 2007 event's cause was an organizational weakness in not implementing the Capacitor Program; Corrective action to prevent recurrence was established to develop a capacitor program; Specified corrective actions for the development of the capacitor program were transferred to other CAs (create a list of effected components), which were subsequently transferred to additional CAs (review the list for inclusion into the capacitor program), and delayed on several occasions; and Long-term CA approval incorrectly assumed the issue requiring evaluation was limited to power supplies in critical systems or considered an enhancement. The inspectors noted that in 2007, a 6-year PM was performed but did not involve the replacement of capacitors, and in January 2009, just prior to an outage period, a specific procedure was created that detailed the requirement to replace the critical commutation capacitors in the inverter. The inspectors determined these activities from 2007 to 2010 represented reasonable opportunities for Entergy staff to (1) identify appropriate maintenance was not being performed on the static inverters, i.e., replacement of the commutation capacitors, C1 and C2, and (2) utilize the vendor manual as a source of information in preparation of maintenance (and troubleshooting) and identify these commutation capacitors in the A4 section of the inverter have a vendor recommended replacement every nine years. Analysis: The inspectors determined that Entergy personnel did not adequately identify and correct in a timely manner a condition adverse to quality to ensure continued availability and reliability of the 31 static inverter. SpeCifically, the static inverter incurred unnecessary unavailability hours and was inoperable for approximately five days following the fuse failure on September 14.2010. Moreover, the static inverter's reliability was impacted during continued operations with capacitors that were beyond the vendor-recommended useful life of 9 years, and it was reasonable for Entergy staff to foresee this condition because the replacement requirement was contained in the vendor manual. The finding was more than minor because the finding was associated with the Mitigating Systems cornerstone attribute of equipment performance and affected the cornerstone objective of ensuring the availability and reliability of systems that respond to initiating events to prevent undesirable consequences. The inspectors evaluated the finding using
S. Prussman Specialist
: IMC 0609, Attachment 4, "Initial Screening and Characterization of Findings." The inspectors determined the finding was of very low Enclosure safety significance because the finding was not a design or qualification deficiency, did not represent a loss of safety function, and was not risk significant with respect to external events. The inspectors determined that this finding had a cross-cutting aspect in the area of Problem Identification and Resolution because Entergy personnel did not implement adequate and timely corrective actions to implement a capacitor program and identify critical capaCitors for replacement prior to failure that resulted in the unavailability of a inverter for approximately five days. [P.1 (d) per I
-Nuclear Safety/Licensing
: MC 031 OJ Enforcement: 10
J. Reynolds Corrective Action Specialist
: CFR 50, Appendix B, Criterion XVI, "Corrective Actions," requires, in part, that the conditions adverse to quality, such as deficiencies and defective material and equipment are promptly identified and corrected. Contrary to the above, Entergy personnel did not correct a condition adverse to quality after identified in 2007 and ensure that commutation capacitors were identified and replaced in a timely manner prior to the occurrence of age-related failures and subsequent unavailability of the 31 static inverter on September 14, 2010. Because this violation is of very low safety significance and has been entered into the Entergy's corrective action program, 2010-02731, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy (NCV 05000286/2010004-01, Untimely Corrective Actions for Degraded Capacitors for the 31 Static Inverter) Maintenance Risk Assessments and Emergent Work Control (71111.13 -4 samples) a. Inspection Scope The inspectors reviewed maintenance activities to verify that the appropriate on-line risk assessments were performed prior to removing equipment for work as required by 10
T. Salentino
: CFR 50.65{a)(4). When planned work scope or schedules were altered to address emergent or unplanned conditions, the inspectors verified that the plant risk was promptly reassessed and managed by station personnel. The documents reviewed during this inspection are listed in the Attachment. The following activities represented four inspection samples: Elevated risk due to Category I thunderstorm and A 1 reactor protection system (RPS) testing on July 19, 2010; Elevated risk for emergent work on 138KV feeder 96952 on July 22, 2010; Elevated risk for troubleshooting 6.9KV Bus 2 with 32 EDG out of service (OOS) on September 10,2010; and Elevated risk with 138KV line 33332 OOS on September 15, 2010. b. Findings No findings were identified. Enclosure 
Superintendent
: R15 Operability Evaluations (71111.15 -4 samples) Resident Quarterly Review a. Inspection Scope The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications. These reviews were conducted to verify that operability determinations were performed in accordance with procedure
-Dry Fuel Storage S. Sandike Sr. HP/Chemical
: ENN-OP-104, "Operability Determinations." The inspectors assessed the technical adequacy of the evaluations to ensure consistency with the UFSAR and associated design and licensing basis documents. The documents reviewed are listed in the Attachment. The following operability evaluations were reviewed and represented four inspection samples: * Radiation monitor R-11 check source failure; * 480V switchgear during control building high temperature; * Residual heat removal pump seal cooling; and * EDG air start system reduced volume. b. Findings No findings were identified. 1R18 Plant Modifications (71111.18 -1 sample) Temporary Modification: Temporarily Disable the Limit Switch for 31 Emergency Diesel Generator (EDG) Fuel Oil Day Tank Inlet Valve
Specialist
: DF-LCV-1207B a. Inspection Scope The inspectors reviewed the temporary modification which disabled the limit SWitch for 31 EDG fuel oil day tank inlet valve
D. Smith Technical
: DF-LCV-1207B while the hydraulic actuator for
Specialist
: LCV-1207B was out of service. Without hydraulic pressure,
F. Spagnuolo
: DF-LCV-1207B fails open in order to ensure fuel oil can always be transferred to any or all of the three fuel oil day tanks. However, with
Supervisor  
: DF-LCV-1207B failed open, the limit switch contact for the valve remains closed, thereby preventing the fuel oil transfer pump from automatically shutting off when the 31 EDG fuel oil day tank has been filled to 90 percent. Entergy's temporary modification disabled the limit switch for
-Control Room M. Tesoriero
: DF-LCV-1207B and permitted the automatic shutoff of the 31 EDG fuel oil transfer pump by relying on the limit switch for 1207A, which is connected in parallel with limit switch for
Manager -Programs and Components
: DF-LCV-1207B. The inspectors reviewed the temporary modification and associated engineering change (EC)-23034 to verify that the temporary modification was conducted in accordance with site procedures, as applicable, including
A Vitale General Manager. Plant Operations  
: EN-DC-136, "Temporary Modifications." The inspectors' review also considered whether the appropriate design interfaces were established during preparation and implementation and were consistent with the design basis information located in the UFSAR. The inspectors also reviewed Entergy's work package that controlled installation of this temporary modification and the associated Enclosure post-installation testing, including the resultant ability of the fuel oil transfer pump to start and secure as required, based on the level of the fuel oil day tanks. b. Findings No findings were identified. 1 Post Maintenance Testing (71111.19 -5 samples) a. Inspection Scope The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems, and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and engineering personnel. The inspectors verified that: test acceptance criteria were clear and the test demonstrated operational readiness consistent with design basis documentation; test instrumentation had current calibrations with the appropriate range and accuracy for the application; and the tests were performed as written, with applicable prerequisites satisfied. Upon completion of the tests, the inspectors reviewed whether equipment was returned to the proper alignment necessary to perform its safety function. Post-maintenance testing was evaluated for conformance against the requirements of 10
: [[contact::R. Walpole Manager]], Licensing
: CFR 50, Appendix B, Criterion XI, "Test ControL" The documents reviewed are listed in the Attachment. The following post-maintenance activities were reviewed and represented five inspection samples: 31 ABFP load sequencer calibration on July 8,2010; 31 EDG maintenance outage on August 10 and 11, 2010; 'B' RPS intermediate range trip block relay failure on August 16, 2010;
: MS-PCV-1135 (32 steam generator atmospheric dump valve) maintenance on August 16 -17,2010; and Feed water low-flow bypass valve (FCV-417L) process signal meter troubleshooting and repair on August 25, 2010. b. Findings No findings were identified. 1 Refueling and Outage Activities (71111.20) Forced Outage 3F010A: Exciter Cooler Leak Repairs and Other Activities a. Inspection Scope The inspectors observed and/or evaluated selected activities during the maintenance outage that was initiated following the manual reactor trip on September 9, 2010, due to Enclosure service water leakage from main turbine generator exciter coolers. These observations and evaluations included: Main unit generator exciter cooler 31 and 32 repairs; TS 3.0.3 entry due to two unavailable off-site sources and one EDG inoperable; 34 reactor coolant pump seal re-seating activities; Carbon dioxide activation due to relief valve lifting on the 31 main boiler feed pump; Initial critic;ality during startup activities on 9f11/201 0; 32 heater drain (HD) pump trip during power ascension and control room personnel response during implementation of abnormal operating procedure on 9/13/2010; and Main turbine overspeed trip and control room personnel response during implementation of abnormal operating procedure on 9/13/2010. b. Findings No findings were identified. 1 Surveillance Testing (71111.22 --4 samples) a. Inspection Scope The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk significant structures, systems, and components, to assess whether test results satisfied technical specifications, UFSAR, technical requirements manual and Entergy procedure requirements. The inspectors verified that: test acceptance criteria were sufficiently clear; tests demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had accurate calibrations and appropriate range and accuracy for the application; tests were performed as written; and applicable test prerequisites were satisfied. Following the tests, the inspectors verified whether equipment was capable of performing the required safety functions. The documents reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented four inspection samples, which included an in-service testing (1ST) surveillance: 0-SOP-LEAK-001, Reactor Coolant System (RCS) Leakrate Surveillance, Evaluation, and Leak Identification, on July 19, 2010; 3-PC-OL27G, Bus 5A 480V Undervoltage Relays Inspection and Calibration, on July 26, 2010; 3-PT-SA045, Main Turbine Stop and Control Valves Test, on July 29,2010; and 3-PT-Q120B, 32 ABFP (Turbine Driven) Surveillance and 1ST, on August 3, 2010. b. Findings No findings were identified. Enclosure 
: OTHER ACTIVITIES Performance Indicator Verification (71151-5 samples) Inspection Scope The inspectors reviewed performance indicator (PI) data listed below to verify the accuracy of the data recorded from July 2009 through June 2010. The inspectors used Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," as applicable, and reviewed associated Entergy procedures and data to verify individual PI accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment. Mitigating Systems Cornerstone Mitigating Systems Performance Index -Emergency AC Power System; Mitigating Systems Performance Index -High Pressure Injection System; Mitigating Systems Performance Index -Heat Removal System; Mitigating Systems Performance Index Residual Heat Removal System; and Mitigating Systems Performance Index -Cooling Water System. No findings were Identification and Resolution of Problems (71152 -2 samples) Routine Problem Identification and Resolution Program Review Inspection Scope As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergy's corrective action program. The review was accomplished by accessing Entergy's computerized database for eRs and attending condition report screening meetings. In accordance with the baseline inspection modules, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for further follow-up and review. The inspectors assessed Entergy personnel's threshold for problem identification, the adequacy of the cause analysis, extent of condition reviews, operability determinations, and the timeliness of the associated corrective actions. No findings were Enclosure 
.2 Annual Sample -Buried Pipe Inspection and Monitoring Program a. Inspection Scol2e The inspectors interviewed the Program Owner (Responsible Engineer) for the Indian Point Buried Pipe Inspection and Monitoring Program and reviewed the related applicable procedures for the program. The inspectors used as a reference the Electric Power Research Institute (EPRI) and NEt guidelines for buried pipe systems. Field observations were made of the areas of past and current buried pipe activities. These included the Unit 2 and Unit 3 condensate storage tank (CST) and auxiliary feedwater (AFW) piping, and the piping exiting the Unit 3 reactor water storage tank to under the independent spent fuel storage installation (ISFSI) haul path. The inspection scope included determining the status and comparison of the site activities and plans to monitor and inspect buried piping and storage tanks. The inspectors ensured these activities met or exceeded the EPRI and NEI guidance and requirements to understand the condition of these components to minimize the occurrence of leakage. Specific documents reviewed during this inspection are listed in the attachment. These activities constitute completion of one in depth problem identification and resolution sample as defined in Inspection Procedure 71152. b. Findings and Observations No findings were identified. A leak in the Unit 2 AFW system 8-inch diameter return line to the CST was identified by Entergy staff on February 15.2009 and repaired. In September 2009. guided wave inspection identified Level 2 G-scan indications in both the Unit 2 and Unit 3 AFW
: CST 12*inch diameter suction lines. Level 2 G-scan indications are areas of moderate interest where follow,.up is recommended. Entergy entered this condition for evaluation into the CAP as
: CR-IP2-2009-00666 . . 3 Annual Sample: Review of Corrective Actions for Emergency Core Cooling Systems (ECCS) Gas Accumulation a. Inspection Scope This inspection focused on Entergy personnel's identification, evaluation, and resolution of deficiencies associated with the accumulation of gas in the ECCS and potential impacts on ECCS equipment, as documented in condition reports during 2007 to 2010. Specifically. a number of condition reports dated 2007 through 2009 documented the requirement to refill the 34 cold-leg injection accumulator due to nitrogen-entrained water leakage into the ECCS. Additionally, condition reports dated 2007 and through 2009 documented rising level in the pressurizer relief tank due to safety injection (51) relief valve 855 lifting while using 31 or 32 SI pumps to refill the COld-leg injection accumulators. Specific condition reports reviewed for these two issues are listed in the attachment to this report. Finally, Entergy
: CR-IP3-2010-01937 documented an Enclosure abnormal pressure increase in the boron injection tank (BIT) and Non-BIT headers following the completion of
: PT-Q134A, 31 RHR Pump Test. The inspectors reviewed operability evaluations and engineering reviews to determine whether Entergy personnel had properly evaluated and dispositioned the operability of the equipment impacted by the issues reviewed. The inspectors reviewed condition reports and an apparent cause analysis to ensure the resolution of the issues were properly classified and prioritized consistent with the safety significance of the issues. The inspectors reviewed completed work orders and planned corrective actions to ensure that actions identified were appropriately focused to correct the problem, and that actions were planned or completed in a timely manner, consistent with the safety significance of the issues. The inspectors reviewed completed work orders and performed a condition report review to ensure actions taken resulted in the correction of the identified problems. Finally, the inspector interviewed the system engineer and reviewed historical condition reports, surveillance procedures, preventative maintenance schedules, gas void detection testing results, industry operating experience to evaluate Entergy's consideration of extent of condition and cause, generic implications, common causes, and previous occurrences of the issues. b. Findings and Observations No findings were identified. The inspectors determined that Entergy personnel properly implemented their corrective action process regarding the identification, evaluation, and resolution of the reviewed issues. The inspectors determined that Entergy's identification of the cause of
: SI-855 lifting and subsequent actions during 3R15 to overhaul and repack
: SI-AOV-890D, 34 cold-leg injection accumulator fill line isolation valve, due to seat leakage was adequate to correct the problem. The inspectors determined that the preventative maintenance schedule for
: SI-855 was appropriate and that the modification implemented to increase the setpoint of
: SI-855 did not negatively impact the ability of the relief valve to protect the system from overpressure. The inspectors determined that Entergy's identification of the cause of 34 cold-leg injection accumulator leakage and subsequent actions to replace check valve
: SI-838D due to seat leakage was adequate to correct the problem. The inspectors determined that while the cause of the abnormal pressure increase in the BIT and Non-BIT headers following the 31 RHR pump test in July 2010 has not been positively identified, Entergy personnel took timely action to assess that the operability of the equipment was not impacted and ruled out certain potential causes. 40A3 Event Follow-Up (71153 -2 samples) (Closed)
: LER 05000286-2009-004-01, Automatic Reactor Trip During Single Feedwater Pump Operation Due to a High 32 Steam Generator Water Level Caused by Inadequate 31 Main Feedwater Pump Governor Valve Setting On May 28, 2009, Unit 3 control room operators responded to an automatic reactor trip that was caused by high level in the 32 steam generator. Subsequently, the cause of the SG water level event was determined by Entergy personnel to be inadequate feedwater controller settings and improper feedwater pump governor valve operation Enclosure .1
associated with the 31 main boiler feedwater pump. Entergy staff entered the issue in the corrective action program as
: CR-IP3-2009-02494 and 02710 and conducted a root . cause evaluation (RCE). Additionally, Entergy submitted
: LER 2009-004-00 in July 2009, which was evaluated and dispositioned as a Finding (FIN) of very low safety significance in NRC inspection report 05000247/2009-005. The inspectors reviewed this supplement LER, which was submitted in April 2010, following revisions to the RCE and associated corrective actions. The inspectors verified the information in the LER was consistent with the updated corrective action program documents. There were no additional findings of significance or violations of NRC requirements identified. This LER is closed . . 2 Manual Reactor Trip on September 9, 2010. due to Exciter Service Water Leak a. Inspection Scope The inspectors evaluated the response of control room personnel following the initiation of a manual reactor trip due to service water identified by operators to be leaking into the main unit generator exciter housing. The inspectors reviewed plant computer data, including the sequence of events report, evaluated plant parameter traces, and discussed the event with plant personnel, to verify that plant equipment responded, as expected, and to ensure that operating procedures were appropriately implemented. The inspectors also verified that station personnel took appropriate actions in response to the unexpected trip of the 34 reactor coolant pump, which was preliminarily determined to be caused by anomalies with the closing sequence of the 6.9kV Bus No. 5/Safety Bus No.2 tie breaker (UT2-ST5) during the fast transfer operation which normally occurs post-trip. The inspectors verified that Entergy's post-trip review group (PTRG) identified the most probable cause of the water that was identified to be leaking into the exciter housing, as well as appropriate recommendations and corrective actions prior.to restart. This event and the PTRG report were entered into Entergy's corrective action program as CR I P3-20 1 0-02682. b. Findings No findings were identified. The inspectors determined that the operational response to the reactor trip was appropriate. The inspectors will conduct future reviews of the root cause evaluation (RCE) and associated corrective actions. These reviews will be conducted following Entergy's submittal of a licensee event report (LER) with regard to the event. Enclosure 
: 40A6 Meetings, Including Exit Exit Meeting Summary On October 28. 2010, the inspectors presented the inspection results to Mr. Joseph Pollock and other Entergy managers and staff, who acknowledged the inspection results. Entergy staff identified documents which were to be considered proprietary and handled as such. AITACHMENT: SUPPLEMENTAL INFORMATION Enclosure 
: SUPPLEMENTAL KEY POINTS OF Entergy Personnel J. Pollock Site Vice President H. Anderson Licensing Specialist V. Andreozzi Systems Engineering Supervisor R. Burroni Systems Engineering Manager P. Conroy Director, Nuclear Safety Assurance J. Dinelli Site Operations Manager J. Lijoi Instrumentation and Controls Superintendent L. Lubrano System Engineer T. McCaffrey Design Engineering Manager D. Morales System Engineer T. Orlando Engineering Director M . Tesoriero Manager Programs and Components A. Vitale General Manager, Plant Operations R. Walpole Licensing Manager LIST OF ITEMS OPENED, CLOSED AND DISCUSSED Opened and Closed 05000247/2010-004-01 NCV Inadequate Identification and Correction of a Condition Adverse to Quality to Ensure the Continued Availability of the Safety-Related No. 31 Static Inverter (Section 1 R12) Closed 050000286/2009-004-01 LER Automatic Reactor Trip During Single Feedwater Pump Operation Due to a High 32 Steam Generator Water Level Caused by Inadequate 31 Main Feedwater Pump Governor Valve Setting (Section 40A3) Attachment 
: LIST OF DOCUMENTS Section 1 R04: Equipment Alignment Procedures 3-COL-CC-1, Component Cooling System, Rev. 28 Section 1 R05: Fire Protection Procedures 3PT-Q130, RES Battery Inspection, Rev. 0
: EN-DC-161, Control of Combustibles, Rev. 4
: PFP-364, Unit 3 Pre-Fire Plan General Floor Plan -Turbine Building -53'-0", Rev. 11
: PFP-392, Outage Support Building -Second Floor, Rev. 5 Pre-Fire Plans
: PFP-351A, AlC Equipment Room -Control Building, Rev. 11
: PFP-355, Lower Electrical Tunnel. Rev. 5
: PFP-356, Lower Electrical Penetration Area, Rev. 0
: PFP-383, Condensate Polisher -Lower Level, Rev. 5
: PFP-384, Condensate Polisher -Upper Level, Rev. 0 Miscellaneous 0090-00066-EVAL-003, Report on Expansion and Seismic Gaps for Indian Point 3 Nuclear Power Plant. dated November 7, 1994
: IP3-RPT-FP-01163, NFPA Code 13-1983 Conformance Review. Rev. 3 Section 1 R07: Heat Sink Performance Procedures
: SEP-SW-001, IPEC NRC G.L 89-13 Service Water Program, Rev. 2 Condition Reports (CR-IP3-) 2010-02384 Work Orders
: 52243920
: 52243921 Miscellaneous 31 EDG Jacket Water and Lube Oil Cooler Inspection Report, dated August 11, 2010 Section 1 R11: Licensed Operator Requalification Procedures
: TQF-210-DD03, LOR Simulator Crew Performance Evaluation Report, Rev.1 Attachment Section 1 R12: Maintenance Effectiveness Procedures 3-IC-PC-I-E-Static Inverter-31, No. 31 Static Inverter Maintenance Procedure, Rev. 0 and Rev. 1 3-IC-SI-27, No. 31 Static Inverter Special Maintenance Procedure, Rev. 9 3-PT-W020, Electrical Verification -Inverters and DC Distribution in Modes 1 to 4, Rev. 12 Condition Reports (CR-)
: IP2-2010-04148
: IP2-2010-04663
: IP3-01674 Calculations
: IP3-CALC-EL-00188, Inverter #31 System Component Sizing Analysis, Rev. 0 Work Orders
: 51438131-02
: 250464
: 248502 Miscellaneous Vendor Manual 498-100000689, Instruction Manual Operations -Maintenance Instructions and Parts Catalog for Elgar Inverters Modellnv. 253-1-106


==Section 1R13: Maintenance Risk Assessment and Emergent Work Control Procedures==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
: EN-WM-104, On Line Risk Assessment, Rev. 2 Completed Procedures 3-ST-M13A, Reactor Protection Logic Channel Functional Test (Shutdown Train A), dated September 10, 2010 Section 1 R15: Operability Evaluations Procedures 3-ARP-013, Panel SKF -Bearing Monitor, Rev. 36 3-PT-Q75A, Functional Test
: RM 11/12, Rev. 18
: ONOP-RM-1, FailUres of Radiation Monitors, Rev.
: EN-OP-104, Operability Determination Process, Rev. Condition Reports 2006-02398 2010-01850 2010-01987 2010-01989 9321-F-27203, Flow Diagram -Auxiliary Coolant System Inside Containment, Rev. 9321-F-27513 Sheet 1, Flow Diagram -Auxiliary Coolant System in PAS and FSB, Rev. Work
: IP3-CALC-CBHV-00997, CB EI. 15'-0" Temperatures at Varying Outdoor Temperatures, Rev. Attachment
: IP3-CALC-ED-01545, 480V Safety Related Switchgear Accident Operation at Above 40 degrees C Ambient, Rev. 0
: JP3-CALC-ED-00301, Evaluation of Short Time Operation of 480V AC Safety Related Switchgear Bus Above 3200A Rating, Rev. 1
: JP3-CALC-ED-00302, Evaluation of Short Time Operation of 480V AC Safety Related Supply Circuit Breaker for Safety Related Switchgear Above 3200A Rating, Rev. 3
: IP3-CALC-ED-01294, 480V Buses 2A. 3A. 5A. and 6A Load vs. Temperature Tables, Rev. 0 Section 1 Ri8: Plant Modifications Procedures
: EN-DC-136, Temporary Plan t Modifications, Rev. 5 Drawings 9321-F-20303. Flow diagram Fuel Oil to Diesel Generators, Rev. 29 9321-LL-31333 Sheet 6, Schematic Diagram Diesel Generator Auxiliaries, Rev. 7 9321-LL-31333 Sheet 15, Schematic Diagram Diesel Generator Auxiliaries, Rev. 6 9321-F-32173, Wiring Diagram Diesel Generators 31-32-33, Rev. 13 Work Orders
: 00240786 Miscellaneous
: EC-23034, Temporarily Disable the "AO" Limit Switch for DF-LCV-1207B


==Section iRi9: Post-Maintenance Testing Completed Procedures==
===Opened and Closed===
: 0-VLV-404-AOV, Use of Air Operated Valve Diagnostics, Rev. 7 3-PT-M13B1, Reactor Protection Logic Channel Functional Test (Reactor Power Greater than 35% -P8), dated August 16, 2010 3-PT-M079A, 31 EDG Functional Test, Rev. 39 3-PT-OL3B1, Auxiliary Boiler Feedwater Pump #31 Load Sequencer Calibration, dated July 8,2010 3-PT-Q120A, 31 Auxiliary Feedwater Pump, dated July 8,2010 3-S0P-EL-001, Diesel Generator Operation, Rev. 42 Condition Reports (CR-IP3-) 2010-02201 Drawings 113E301 Sheet 3, Reactor Protection System Schematic Diagram, Rev. 10 113E301 Sheet 4, Reactor Protection System Schematic Diagram, Rev. 10 Work Orders
: 05000247/2010-004-01 . NCV Reactor Trip Breaker Preventative
: 00143710
Maintenance
: 00245038
Procedure
: 00246268
was not Adequately
: 00246271
Implemented (Section 1 R19)
: 51692331
===Closed===
: 52244274
: 05000247/2010-004-00
: 52257653
: LER Plant Operation
: 52259198
: Outside Technical
: 52266847 Attachment Section 1 R20: Refueling and Outage Activities Procedures 3-AOP-TURB-1, Main Turbine Trip Without a Reactor Trip, Rev. 5 3-AOP-FW-1, Loss of Feedwater, Rev. 7 3-POP-1.2, Reactor Startup, Rev. 51 3-POP-2.1, Operation at Greater Than 45% Power, Rev. 54 Section 1 R22: Surveillance Testing Procedures 0-OSP-TG-001, Main Turbine Stop and Control Valve Contingency Actions, Rev. 0 O-SOP-LEAKRA
: Specifications
: TE-001, ReS Leakrate Surveillance, Evaluation, and Leak Identification, Rev. 1 Completed Procedures 0-SOP-LEAKRATE-001, RCS Leakrate Surveillance, Evaluation, and Leak Identification, dated July 9,2010 3-PC-OL27G, Bus 5A 480 Volt Undervoltage Relays Inspection and Calibration, Rev. 1 3-PT-Q120B. 32 ABFP (Turbine Driven) Surveillance and 1ST, Rev. 16 3-PT-SA045, Main Turbine Stop and Control Valves Exercise Test. Rev. 4 Condition Reports (CR-IP3-) 2010-02037 2010-02055
: Due to a Leak in the Reactor Coolant Pressure Boundary (Section 40A3) Attachment 


==Section 40A1: Performance Indicator Verification Procedures==
==LIST OF DOCUMENTS==
: 3-S0P-CC-001 B, Component Cooling System Operation. Rev. 33 3-ARP-009, Panel SFF -Chemical and Volume Control System, Rev. 38
REVIEWED Common Documents Indian Point Unit 2 Control Room Narrative Indian Point Unit 2 Individual Plant Indian Point Unit 2 Individual Plant Examination of External Indian Point Unit 2 Plan of the Indian Point Unit 2 Technical Requirements Indian Point Unit 2 Technical Specifications and Indian Point Unit 2 Updated Final Safety Analysis Section 1 R01: Adverse Weather Protection 
: EN-Ll-114, Performance Indicator Process, Rev. 4 Completed Procedures
===Procedures===
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator High Pressure Injection, dated October 2, 2009
: 2-AOP-FLOOD-1, Flooding, Rev. 6
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator High Pressure Injection, dated January 7, 2010
: IP-SMM, Event Notification and Reporting, Rev. 11
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator High Pressure Injection. dated April 3, 2010
: OAP-008, Severe Weather Preparations, Rev. 7 Condition Reports (CR-IP2-)
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator High Pressure Injection. dated July 8, 2010
: 2010-04578 
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Residual Heat Removal, dated October 2,2009
===Miscellaneous===
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Residual Heat Removal, dated January 7, 2010
: 50.72 Event Notification
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Residual Heat Removal, dated April 3, 2010
: 46092, July Individual Plant Examination for External Events for Indian Point Unit 2, Section Evaluation of Flood Area
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Residual Heat Removal, dated July 8, 2010
: PAS 68-1
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Heat Removal, dated October 6, 2009 Attachment
: IP-RPT-04-00230, Indian Point Unit 2 Probabilistic Safety Assessment, Rev. 1 Section 1 R04: Equipment Alignment 
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Heat Removal, dated January 6, 2010
===Procedures===
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Heat Removal, dated April 2, 2010
: 2-ARP-SMF, CCR Safety Injection, Rev. 22 2-COL-4.2.1, Residual Heat Removal System. Rev. 27 2-COL-10.0, Locked Safeguards Valves. Rev. 40 2-COL-10.1.1, Safety Injection System, Rev. 33 2-COL-18.1, Main Steam and Reheat System, Rev. 38 2-COL-21.3, Steam Generator Water Level and Auxiliary Boiler Feedwater, Rev. 30 2-PT-2Y020A, 21 SICP Comprehensive Test, Rev. 1 2-S0P-1 0.1.1, Safety Injection Accumulators and Refueling Water Storage Tank Operations, Rev. 52
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Heat Removal, dated July 6,2010
: OAP-019, Component Verification and System Status Control. Rev. 5 Condition Reports (CR-IP2-)
: EN-L1-114, Performance Indicator Process --Mitigating Systems Performance Indicator Emergency AC Power, dated October 6, 2009
: 2008-05043 
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Emergency AC Power, dated January 7, 2010
===Drawings===
: EN-Ll-114, Performance Indicator Process --Mitigating Systems Performance Indicator Emergency AC Power, dated April 5, 2010
: 9321-F-2735, Safety Injection System, Rev. 140 Section 1 R05: Fire Protection 
: EN-Ll-114, Performance Indicator Process --Mitigating Systems Performance Indicator Emergency AC Power, dated July 7,2010
===Procedures===
: EN-Ll-114, Performance Indicator Process --Mitigating Systems Performance Indicator Cooling Water Support (Component Cooling Water). dated October 5,2009
: IP2-RPT-03-00015, IP2 Fire Hazards Analysis, Rev. 2 Condition Reports (CR*IP2*)
: EN-L1-114, Performance Indicator Process --Mitigating Systems Performance Indicator Cooling Water Support (Component Cooling Water), dated January 7,2010
: 2010-04515
: EN-L1-114, Performance Indicator Process --Mitigating Systems Performance Indicator Cooling Water Support (Component Cooling Water), dated April 4. 2010
: 2010*05048
: EN-Ll-114, Performance Indicator Process -Mitigating Systems Performance Indicator Cooling Water Support (Component Cooling Water), dated July 6,2010
: 2010-05075
: EN-U-114, Performance Indicator Process -Mitigating Systems Performance Indicator Cooling Water Support (Service Water), dated October 7,2009
: Pre Fire Plan
: EN-U-114, Performance Indicator Process --Mitigating Systems Performance Indicator Cooling Water Support (Service Water), dated January 7,2010
: PFP-160A, Appendix RlStation Black Out Emergency Diesel Generator Unit 1 -33'-0" Elevation, Rev.
: EN-Ll-114, Performance Indicator Process --Mitigating Systems Performance Indicator Cooling Water Support (Service Water), dated April 4, 2010
: PFP-205, Primary Auxiliary Building -35'*0" Elevation, Rev.
: EN-Ll-114, Performance Indicator Process --Mitigating Systems Performance Indicator Cooling Water Support (Service Water), dated July 8,2010
: PFP-208, Primary Auxiliary Building -68'-0" Elevation, Rev.
: PFP-209, Primary AUXiliary Building -68'-0" Elevation, Rev.
: PFP-259, Auxiliary Feedwater Pump Room -18" Elevation, Rev. Miscellaneous
: EN-DC-161, Control of Combustibles, Rev. 4 Section 1 ROG: Flood Protection Measures Procedures
: 2-AOP-FLOOO-1, Flooding, Rev. 6
: OAP-008, Severe Weather Preparations, Rev. 7 Condition Reports (CR-IP2-)  
: 2009-00456 
===Drawings===
: 9321-F-2719-134, Waste Disposal System, April 14, 2006 Miscellaneous 
===Design Basis Document===
for Component Cooling Water System, Rev. 1 Individual Plant Examination for External Events for Indian Point Unit 2, Section 5.2.2.1.3, Evaluation of Flood Area
: PAB 68-1
: IP-RPT-04-00230, Indian Point Unit 2 Probabilistic Safety Assessment, Rev. 1 UFSAR Section 11.1, Waste Disposal System, Rev. 21 Section 1 R11: Licensed Operator Requalification Program Procedures
: 2-E-3, Steam Generator Tube Rupture, Rev. 1 2-FR-S.1, Response to Nuclear Power Generation/Anticipated Transient Without SCRAM, Rev. 1
: OAP-008, Severe Weather Preparations, Rev. 7 Attachment


==Section 40A2: Identification and Resolution of Problems Procedures==
==Section 1R12: Maintenance==
: 3-PT-M108, RHRlSI/CS System Venting, Rev. 11
: Effectiveness 
===Procedures===
: 2-ARP-025.
: Station Auxiliary Transformer, Rev. 1 Condition Reports
: 2008-01258
: 2008-02723
: 2008-02954
: 2009-00419
: 2009-01284
: 2010-02994
: 2010-03173 
===Work Orders===
: 152061
: 234069
: 51324390
: 138 KV System Health Report, January -June, IPEC Combined Basis Document for 138 KV System, Rev. Operational Decision Making Instruction, Reactor Coolant Pump 21 Upper Oil Elevated Bearing Temperatures, June
: 29, Operations Narrative Logs -July 26, Reactor Coolant Pump 21 Upper Thrust Bearing Temperature Trend, June 23, September
: 2, 201 R&G Laboratories, Oil Analysis Severity for Reactor Coolant Pump 21, August 11, Section 1 R13: Maintenance Risk Assessments and Emergent Work Control Procedures
: 2-PT-M048, 480 Volt Undervoltage Alarm, Rev. 23 2-S0P 24.1.1, Service Water Hot Weather Operation, Rev. 11
: EN-WM-104, On Line Risk Assessment, Rev. 1
: IP-SMM-1 01, Online Risk Assessment, Rev. 3
: OAP-008, Severe Weather Preparations, Rev. 6 Condition Reports (CR-IP2-)
: 2008-03893
: 2009-00154 
===Miscellaneous===
: Daily Status Report, Indian Point 2, August 24, 2010
: DRN 10-4007, 2-PT-M048
: Test Switch Monitor, Rev. 6 Operator Narrative Logs, July 19, 2010 Operator Narrative Logs, August 19, 2010 Operator Narrative Logs, August 24, 2010 Operator Narrative Logs, September
: 16,2010 Operator's Risk Report, July 19,2010 Operator's Risk Report, August 19, 2010 Operator's Risk Report, August 24, 2010 Operator's Risk Report, September
: 16, 2010 Technical Specification
: 3.3.5, Loss of Power Diesel Generator Start Instrumentation Technical Specification
: 3.8.1, AC Sources -Operating Updated Final Safety Analysis Report, Section 7.5.2.1.12, Bus Undervoltage, Rev. 21 Attachment
 
==Section iRi5: Operability==
: Evaluations
: 2-ARP-SJF, Cooling Water and Air, Rev.
: EN-OP-104, Operability Determination Process, Rev. Condition Reports
: 2006-07329
: 2010-04457
: 2010-04631'
: 2010-04711
: 2010-04753
: 2010-05173 
===Condition Reports===
: 2006-04063
: 2008-00698
: Work
: 247502
: 21-F-4017, Control Building Heating Vent and Air Conditioning, Rev.
: GMH-00033-00, Indian Point 480V Switchgear Room Ventilation in the Event Some Dampers are Shut or in Closed Position, Rev.
: IP-06-00329, Replacement of EDG Air Start Motors, Rev. Miscellaneous
: 2-ARP-003, Diesel Generator, Rev. 8 Emergency Diesel Generator Air Receiver Pressure Trends, July 2008 -July 2010 lO-lAR-2010-123, License Amendment Request for non-conservative technical specification
: NRC Administrative letter 98-10, Dispositioning of Technical Specifications that are Insufficient to Assure Plant Safety NRC Inspection Manual, Part 9900: Technical Guidance, Operability Determinations and Functionality Assessments for Resolution of Degraded or Nonconforming Conditions Adverse to Quality or Safety, April 16, 2008 Technical Specification
: 3.8.3.F, Diesel Fuel Oil and Starting Air Standing Order 06-04, Non-Conservative Technical Specification
: 3.8.3.F
 
==Section iRi8: Plant Modifications==
 
===Procedures===
: 2-AOP-RCP-1, Reactor Coolant Pump Malfunction, Rev. 10 2-ARP-SCF, Condensate and Boiler Feed. Rev. 42
: EN-DC-136, Temporary Modifications, Rev. 5
: EN-LJ-100, Process Applicability Determination, Rev. 9 Condition Reports (CR-IP2-)
: 2010-04805
: 2010*04869 
===Work Orders===
: 245127 Attachment
===Miscellaneous===
: EC-23681, Raise 21 RCP Bearing Temperature Alarm Setpoint from 185F to 190F and Manual Trip Setpoint from 200F to 205
 
==Section 1R19: Post-Maintenance==
: Testing
: 0-MS-412, Inspection and Cleaning of Bus Bars, Contacts, Ground Connections, Wiring Insulators, Rev. 2-PT-M21A, Emergency Diesel Generator Load Test, Rev. 2-PT-M7, Analog Rod Position Functional, Rev. 2-PT-W020, Electrical Verification
-Inverters and DC Distribution in Modes 1 to 4, Rev. 2-S0P-27.1.5, 480 Volt System, Rev.
: EN-Ll-119, Apparent Cause Evaluation Process, Rev. Completed 
===Procedures===
: 0-IC-SI-69, DAM502 Dual Alarm Module Replacement, Rev. 9, September
: 7, 2010 0-PMP-409-CVCS, Replacement of Fluid Cylinder Valves -Union
: QX-300 Charging Pump, Rev. 2, July 21, 2010 0-PMP-413-CVCS, Inspection/Replacement of Charging Pump Fluid Cylinder Stuffing Box Seals, Rev. 2, July 21, 2010 2-PT-Q58, Steam Generator Level Bistables, Rev. 15, September
: 7,2010 Condition Reports (CR-IP2-)
: 2001-00908 2003-04862 2007-00577
: 2009-00010
: 2010-04451
: 2010-04453
: 2010-04557
: 2010-04699
: 2010-04720
: 2010-04816
: 2010-04864
: 2010-05163
: 2010-05208
: 2010-05317
: 2010-05399 2010-05698 2010-05772 2010-05776 2010-05790 2010-05795 
===Work Orders===
: 174427
: 174427
: 2419
: 242655
: 242656
: 246479
: 51661337 Drawing 110E073, Reactor Breaker Schematic, Rev. 28 Miscellaneous Elgar Static Inverter Vendor Manual Emergency Diesel Generator Maintenance Outage Schedule, September
: 16, 2010 Technical Specification
: 3.1.7, Rod Position Indication Unit 2 -118V Instrument Bus System Health Report, 2 nd Qtr 2010 Section 1 R20: Refueling and Outage Activities 
===Procedures===
: 2-POP-1.2, Reactor Startup, Rev. 54 2-POP-1.3, Plant Startup from Zero To 45% Power, Rev. 81 2-POP-2.1, Operation at Greater Than 45% Power, Rev. 57 Attachment 
: 2-POP-3.1, Plant Shutdown from 45% Power, Rev. 2-POP-3.3, Plant Cooldown -Hot to Cold Shutdown, Rev. 2-PT-R156, Reactor Coolant System Boric Acid Leakage and Corrosion Inspection, Rev. 2-S0P-21.1, Main Feedwater System, Rev.
: EM-OM-123, Fatigue management Program, Rev. Condition Reports
: 2010-05519 2010-05696
: Work EmpCenter Fatigue Management Oil Analysis for 21 Reactor Coolant Pump, August 11, Operational Decision Making Instruction for 21 Reactor Coolant Pump, June 29, Outage Schedule for 21 Reactor Coolant Pump Repairs, July Trend for 21 Reactor Coolant Pump Bearing Temperatures, June 23 -September
: 3, Section 1 R22: Surveillance Testing Procedures
: 2-PT-M048, 480 Volt Undervoltage Alarm, Rev. 23 2-S0P-3.1, Charging, Seal Water, and Letdown Control, Rev. 66
: EN-WM-104, Online Risk Assessment, Rev. 0 Completed 
===Procedures===
: 2-PT-Q58, Steam Generator Level Bistables, Rev. 15, August 4,2010 2-PT-Q62, High Steam Flow and Turbine First Stage Pressure Bistables, Rev. 15, . June 30, 2010 2-PT-Q88, CCW Check Valve 790 and Stroke Testing of Valves 791, 798 & 796, 793, Rev. 6, July 30, 2010 Condition Reports (CR-IP2-)
: 2001-08968
: 2008-02231
: 2008-03893
: 2010-00846
: 2010-03430
: 2010-04365
: 2010-04888
: 2010-04928
: 2010-04952 
===Work Orders===
: 52223773
: 52242119
: 253836 Calculation
: FIX-000132, Steam Generator Narrow Range Instrument Loop Accuracy/SetpointiUncertainties, Rev. 0 Miscellaneous
: DRN 10-4007, 2-PT-M048
: Test Switch Monitor, Rev. 6 Operator Narrative Logs, August 19,2010 Operator's Risk Report, August 19, 2010 Attachment Technical Specification
: 3.3.5, loss of Power Diesel Generator Start Technical Specification
: 3.S.1, AC Sources -
: Updated Final Safety Analysis Report, Section 7.5.2.1.12, Bus Undervoltage, Rev. Section 1 EP6: Drill Evaluation
: IPEC-EP, Indian Point Emergency Plan, Rev. Condition Reports
: 2001-05584
: 2010-05444
: 2010-05445
: 2010-05461
 
==Section 40A1: Performance==
: Indicator Verification
: EN-Ll-114, Performance Indicator Process, Rev.
: High Pressure Injection
: PRA Model Update -January 10, Mitigating Systems Performance Indicator Basis Document, Rev. Mitigating Systems Performance Indicator Consolidated Data Entry Reports -High Injection, July 2009 -June 2010 Mitigating Systems Performance Indicator Consolidated Data Entry Reports -Residual Heat Removal, July 2009 -June 2010 Operator Narrative logs, July 2009 -June 2010 Residual Heat Removal PRA Model Update, January 10, 2008 System Health Reports -High Pressure Injection, July 2009 -June 2010 System Health Reports -Residual Heat Removal, July 2009 -June 2010
 
==Section 40A2: Identification==
 
and Resolution of Problems Procedures
: CEP-BPT-0100, Buried Piping and Tanks Inspection and Monitoring, Rev. 0
: CEP-BPT-0100, Buried Piping and Tanks Inspection and Monitoring, Rev. 0
: EN-DC-167, Classification of Structures, Systems, and Components, Rev. 4
: EN-DC-343, Buried Piping and Tanks Inspection and Monitoring Program, Rev. 2
: EN-DC-343, Buried Piping and Tanks Inspection and Monitoring Program, Rev. 2
: EN-DC-167. Classification of Structures, Systems, and Components, Rev. 4
: EN-EP-S-002-MUl
: EN-EP-S-002-MULTI, Buried Piping andTanks General Visual Inspection. Rev. 0
: TI, Buried Piping and Tanks General Visual Inspection, Rev. 0
: EN-IS-112, Trenching, Excavating and Ground Penetrating Activities, Rev. 6 IPEC U2 and U3 Buried Pipe and Tank Inspections summary for October 12, 2008 to March 31, 2010 Condition Reports (CR-)
: EN-IS-112, Trenching, Excavating and Ground Penetrating Activities, Rev. 6 Entergy Buried PipinglTanks Action Plan, Rev. 3 IPEC Buried Piping and Tank Program Health Report for July 2009 -September
: IP2-2008-04754
: 2009, as updated to July 6,2010 IPEC U2 and U3 Buried Pipe and Tank Inspections summary for October 12,2008 to March 31, 2010 IPEC U2 and U3 Safety Related and Rad fluid piping lists. Condition Reports  
: IP2-2009-00666
: 2008-04754  
: IP2-2010-01146
: 2009-00666  
: IP3-2007-00019
: 2010-00537 
: IP3-2007*00247
===Condition Reports===
: IP3-2007 -00487
: 400428. Appendix R Emergency Lighting Safe Shutdown Paths Emergency lighting Rev. Miscellaneous
: IP3-2007-00489
: EPRI Report
: IP3-2007 -00504
: 1016456, Recommendations for an Effective Program to Control the Degradation of Buried Inspection Report for AFW lines 1505. 1509 and 10" overflow, IPU2, December 4,
: IP3-2007 -00508
: NEI 09-14, Guidance for the Management of Buried Piping Integrity, January Report
: IP3-2007-01162
: IP-RPT-09-00011, Corrosion  
: IP3-2007-01546
: ICathodic Protection Field Survey and Assessment Underground Structures at IP U2 and U3. Rev. 0, October Root Cause Analysis Report for
: IP3-2007-03211
: CR-IP2-2009-00666, May SIA Report of G-Scan Assessment of various Buried pipe sections at IP U2 and September  
: IP3-2007-04168
: 23-24, 2009
: IP3-2008-00875
 
: IP3-2008-01100
==Section 40A3: Event Follow-up==
: IP3-2008-01656
: 2-DCS-009-GEN, MPC Transfer &
: IP3-2008-02234
: HI-STORM Movement, Rev. 2-IC-PC-N-P-408A, Main Boiler Feed Pump Discharge Pressure Speed Control, Rev. 0 &
: IP3-2008-02277
: IP-EP-AD13, IPEC Emergency Plan Administrative Procedures, Rev.
: IP3-2009-00061
: IP-SMM-OP-105, Post Transient Evaluation, Rev. Completed 
: IP3-2009-01152
===Procedures===
: IP3-2009-01640
: 2-PT-M49A, Appendix R Emergency Lighting (Conventional).
: IP3-2010-01937 Attachment
: Rev. 22, August 3,2010 2-PT-M49B, Appendix R Emergency lighting (Nuclear), Rev. 14, August 3,2010 2-PT-R156, RCS Boric Acid Leakage and Corrosion Inspection, Rev. 1
===Drawings===
: IP-SMM-OP-105, Post Transient Evaluation, Rev. 6, September  
: 9321-F-27353, Flow Diagram Safety Injection System Sheet No.1, Rev. 41 9321-F-27503, Flow Diagram Safety Injection System Sheet No.2, Rev. 50 Work Orders
: 3, 2010 Condition Reports (CR-IP2-) 2010-05082 2010-05484
: 00136869
: 2010-05487
: 00169294 Miscellaneous EPRI Report
: 2010-05494
: 1016456, Recommendations for an Effective Program to Control the Degradation of Buried Pipe Inspection Report for AFW lines 1505, 1509 and 10" overflow. IPU2, December 4, 2008
: 2010-05496
: NEI 09-14, Guidance for the Management of Buried Piping Integrity, January 2010 Report
: 2010-05587
: IP-RPT-09-00011, Rev 0, Corrosion ICathodic Protection Field Survey and Assessment of Underground Structures at IP U2 and U3, Rev. 0, October 2008 Root Cause Analysis Report for
: 2010-01631 
: CR-IP2-2009-00666, May 14, 2009 SIA Report of G-Scan Assessment of various Buried pipe sections at IP U2 and U3, September 23-24, 2009 NRC Inspection Report 05000286/201011 IPEC U2 and U3 Safety Related and Rad fluid piping lists Entergy Buried PipinglTanks Action Plan, Rev 3 IPEC Buried Piping and Tank Program Health Report for July 2009 -September 2009, as updated to July 6,2010 Attachment
===Work Orders===
: 182848-02 
===Miscellaneous===
: Engineering Correspondence, Inspection of Dry Cask Components Pertaining to Stuck MPC Condition, August 17, 2010 Entergy letter from Clay Wilson, IPEC System Engineering.
to Holtec International dated August 17,2010, Subject: Inspection of Dry Cask Components pertaining to stuck MPC condition, August 12. 2010 Holtec International letter to Tim Salentino, IPEC, Subject: Resumption of MPC transfer at IP2, August 18, 2010 Holtec International letter to Tim Salentino, IPEC, Subject: Structural and Thermal review of Stuck MPC condition at IP2, August 16,2010 Holtec Letter, Resumption of MPC Transfer at IP2, August 18, 2010 Holtec Letter, Structural and Thermal Review of Stuck MPC Condition at IP2, August 16, 2010 Attachment 
: IPEC Procedure Review and Approval Form
: IP-SMM-AD-102, Rev. 6, for Procedure
: MPC Transfer &
: HI-STORM Movement, No. 2-DSC-009-GEN, Rev. 8 Operator Narrative Logs, September
: 3, 2010 Attachment
: 2R19 ACE ADAMS AFW CAP CFR CR CST EC EDG EL EPRI FSAR IMC ISFSI LER MPC NCV NEI NRC PFP PI PM PMT PTRG ,QP RCP RCS RCE RPS RTB SSC ST TS UFSAR URI WO A-11
==LIST OF ACRONYMS==
==LIST OF ACRONYMS==
: [[ADAMS]] [[]]
Spring 2010 refueling
: [[ABFP]] [[]]
outage Apparent Cause Evaluation
: [[AFW]] [[]]
Agency Wide Document Management
: [[CA]] [[]]
System Auxiliary
: [[BIT]] [[]]
Feedwater ,Corrective
: [[CAP]] [[]]
Action Program Code of Federal Regulations
: [[CCW]] [[]]
Condition
: [[CFR]] [[]]
Report Condensate
: [[CR]] [[]]
Storage Tank Engineering
: [[CS]] [[]]
Change Emergency
: [[CST]] [[]]
Diesel Generator
: [[ECCS]] [[]]
Emergency
: [[EDG]] [[]]
Light Electric Power Research Institute
: [[ENTERG]] [[Y]]
Final Safety Analysis Report Inspection
: [[EPRI]] [[]]
Manual Chapter Independent
: [[FIN]] [[]]
Spent Fuel Storage Installation
: [[HD]] [[]]
Licensee Event Report Multipurpose
: [[IMC]] [[]]
Canister Non-Cited
: [[IPEC]] [[]]
Violation
: [[LER]] [[]]
Nuclear Energy Institute
: [[MBFP]] [[]]
Nuclear Regulatory
: [[NDE]] [[]]
Commission
: [[NEI]] [[]]
Pre-Fire Plan Performance
: [[NRC]] [[]]
Indicator
: [[NCV]] [[]]
Preventive
: [[NUREG]] [[]]
Maintenance
: [[OOS]] [[]]
Post Maintenance
: [[PFP]] [[]]
Test Post-trip
: [[PI]] [[]]
Review Group Augmented
: [[PM]] [[]]
Quality Reactor Coolant Pump Reactor Coolant System Root Cause Evaluation
: [[PT]] [[]]
Reactor Protection
: [[RG]] [[]]
System Reactor Trip Breaker Structures, Systems, and Components
: [[RCE]] [[]]
Surveillance
: [[RCP]] [[]]
Test Technical
: [[RCS]] [[]]
Specifications
: [[RES]] [[]]
Updated Final Safety Analysis
: [[RHR]] [[]]
Report Unresolved
: [[RPS]] [[]]
Item Work Order Attachment
: [[SI]] [[]]
: [[SSC]] [[]]
: [[TS]] [[]]
: [[UFSAR]] [[Agency Wide Document Management System Auxiliary Boiler Feed Pump Auxiliary Feedwater System Corrective Action Boron Injection Tank Corrective Action Plan Component Cooling Water Code of Federal Regulations Condition Report Containment Spray Condensate Storage Tank Emergency Core Cooling Systems Emergency Diesel Generator Entergy Nuclear Northeast Electric Power Research Institute Finding Heater Drain Inspection Manual Chapter Indian Point Energy Center License Event Report Main Boiler Feed Pump Non-Destructive Examination Nuclear Energy Institute Nuclear Regulatory Commission Non-Cited Violation NRC Technical Report Designation Out of service Pre-Fire Plan Performance Indicator Preventive Maintenance Post-Trip Review Group Root Cause Evaluation Reactor Coolant Pump Reactor Coolant System Radiological and Environmental Services Residual Heat Removal Reactor Protection System Safety Injection Structures, Systems, and Components Technical Specification Updated Final Safety Analysis Report Attachment]]
}}
}}

Revision as of 06:30, 20 August 2018

IR 05000247-10-004, on 07/01/2010 - 09/30/2010, Indian Point Nuclear Generating, Indian Point, Unit 2, Post-Maintenance Testing
ML103140355
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 11/10/2010
From: David Lew
Reactor Projects Branch 2
To: Pollock J E
Entergy Nuclear Operations
Gray, Mel NRC/RGNI/DRP/PB2/610-337-5209
References
EA-10-212 IR-10-004
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UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406*1415 November 10. 2010 EA-10-212 Mr. Joseph Site Vice President Entergy Nuclear Operations, Inc. Indian Point Energy Center 450 Broadway, GSB Buchanan, NY 105110249 INDIAN POINT NUCLEAR GENERATING UNIT 2 -NRC INTEGRATED INSPECTION REPORT 05000247/2010004 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Pollock:

On September 30,2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report documents the inspection results, which were discussed on October 28, 2010, with you and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents one self-revealing finding of very low safety significance (Green). This finding was determined to involve a violation of NRC reqUirements.

However, because of its very low safety significance and because it was entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. Additionally, if you disagree with the cross-cutting aspect assigned to the finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. r I In addition, the inspectors reviewed Licensee Event Report 05000247/2010-004, which described the circumstances associated with reactor coolant system pressure boundary leakage from a five-sixteenth inch through-wall weld defect located at a socket weld associated with the 22 reactor coolant pump three-quarter inch seal bypass line. Although this issue constitutes a violation of NRC requirements, in that any reactor coolant system boundary leakage at power constitutes a violation, the NRC concluded that this issue was not within Entergy's ability to foresee and correct, that Entergy staff's actions did not contribute to the degraded condition, and that actions taken were reasonable to identify and address this matter. As a result, the NRC did not identify a performance deficiency.

A risk evaluation was performed and the issue was determined to be of very low safety significance.

Based on these facts, I have been authorized, after consultation with the Director, Office of Enforcement, and the Regional Administrator, to exercise enforcement discretion in accordance with Section 3.5 of the Enforcement Policy and refrain from issuing enforcement for the violation.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of from the Publicly Available Records component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room). David C. Lew, Director DiviSion of Reactor Projects Docket No. 50*247 License No. DPR-26

Enclosure:

Inspection Report No. 05000247/2010004 wI

Attachment:

Supplemental Information cc w/encl: Distribution via ListServ Enclosure J. 2 In addition, the inspectors reviewed licensee Event Report which described the circumstances associated with reactor coolant system pressure boundary leakage from a five-sixteenth inch weld defect located at a socket weld associated with the 22 reactor coolant pump inch seal bypass line. Although this issue constitutes a violation of NRC requirements, in that any reactor coolant system boundary leakage at power constitutes a violation, the NRC concluded that this issue was not within Entergy's ability to foresee and correct, that Entergy staffs actions did not contribute to the degraded condition, and that actions taken were reasonable to identify and address this matter. As a result, the NRC did not identify a performance deficiency.

A risk evaluation was performed and the issue was determined to be of very low safety significance.

Based on these facts, I have been authorized, after consultation with the Director, Office of Enforcement, and the Regional Administrator, to exercise enforcement discretion in accordance with Section 3.5 of the Enforcement Policy and refrain from issuing enforcement for the violation.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of from the Publicly Available Records component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at Public Electronic Reading Room).

Sincerely,IRA! David C. Lew, Director Division of Reactor Projects Docket No.

license No. DPR-26 Inspection Report No. 05000247/2010004 wI

Attachment:

Supplemental Information Distribution (via W.Dean, RA R. Conte, DRS M. Catts, M. Dapas. D. Holody, ORA ) A. Ayegbusi, RI D. Lew. G. Miller, RI OEDO D. Hochmuth, DRP J. Clifford.

DRP M. Gray. D. Bearde, DRS D. Collins, B. Bickett, DRP RidsNrrPMlndianPoint Resource D. Roberts. S. McCarver.

DRP RidsNrrDorlLpl1-1 Resource P. Wilson. M. Jennerich, DRP ROPreport Resource@nrc.gov SUNSI Review Complete:

bb (Reviewers Initials)

ML 103140355 DOCUMENT NAME: G:\DRP\BRANCH2\a

-Indian Point 2\1nspection Reports\lP2 IR 201 0-004\IP2 201 0.004.final.docx After declaring this document "An OffICial Agency Record" it will be released to the Public. To receive a copy of this document, indicate in the box: "C" =Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RIIDRP Ilhp RI/DRP I RIIORA NAME MCatts/mc BBickettlbb DHolody/mmm DATE 10125/10 10/25/10 OFFICE RIIDRS I RIIDRP I RIIDRP NAME RConte/rc MGray/mQ DATE 10126/10 11/03/10 OFFICIAL RECORO COpy ,.

Docket No.: License No.: Report No.: Licensee:

Facility:

Location:

Dates: Inspectors:

Approved By: U.S. Nuclear Regulatory Region Entergy Nuclear Northeast Indian Point Nuclear Generating Unit Buchanan, NY July 1, 2010 through September M. Catts, Senior Resident Inspector

-Unit O. Ayegbusi, Resident Inspector

-Unit B. Bickett, Senior Project Engineer -Region H. Gray, Senior Reactor Inspector

-Region J. Nicholson, Health Physicist

-Region Mel Gray, Projects Branch Division of Reactor Enclosure 2

SUMMARY OF FINDINGS

IR 05000247/2010004; 7/01/2010

-9/30/2010;

Indian Point Nuclear Generating (Indian Point) Unit 2; Post-Maintenance Testing. This report covered a three-month period of inspection by resident and region-based inspectors.

One non-cited violation (NCV) of very low significance (Green) was identified.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process." The cross-cutting aspect for the finding was determined using IMC 0310, "Components within the Cross-Cutting Areas." Findings for which the significance determination process does not apply may be Green, or be assigned a severity level after NRC management review. The NRC's program for overseeing safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

Cornerstone: Mitigating

Systems

Green.

A self-revealing NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures and Drawings," was identified because Entergy personnel did not adequately implement the preventive maintenance (PM) procedure for the B reactor trip breaker (RTB}.Specifically, on March 10,2009, Entergy staff did not adequately implement PM Procedure 0-BRK-401-ELC, 'Westinghouse, Reactor Trip and Bypass Circuit Breaker (DB-50)," which resulted in the inoperability of the B RTB shunt trip device function on July 5, 2010. Entergy personnel took immediate corrective actions to replace the B RTB and its associated fuse block assembly.

This issue was entered into Entergy's corrective action program as condition report (CR)-IP2-201 0-4451. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems cornerstone and affects the cornerstone objective of ensuring the availability and reliability of systems that respond to initiating events to prevent undesirable consequences (Le. core damage). Specifically, inadequate preventive maintenance contributed to the failure of the shunt trip device function of the B RTB. Using IMC 0609.04, "Phase 1 -Initial Screening and Characterization of Findings," the finding was determined to have very low safety Significance (Green) because the finding did not result in a loss of system safety function because the undervoltage coil was operable; there was not an actual loss of safety function of a single train for greater than its technical speCification allowed outage time; and the issue was not potentially risk significant due to a seismic, flooding, or severe weather initiating event. The finding has a cross-cutting aspect in the area of problem identification and resolution associated with the corrective action program attribute of complete and accurate identification of issues. Specifically, Entergy staff performing preventive maintenance did not identify and communicate RTB conditions completely and accurately such that the B RTB conditions were fully identified in the CAP. P.1(a) per IMC 0310] (Section 1R19)

4

REPORT DETAILS

Summary of Plant Status Indian Point Unit 2 began the inspection period operating at full reactor power (100%). The Unit 2 reactor automatically tripped during a planned shutdown on September 3,2010, due to high water level in the 23 steam generator.

Unit 2 remained shutdown for a planned maintenance outage to repair the 21 reactor coolant pump (RCP) motor. Operators returned the plant to full power on September 15, 2010. Unit 2 remained at or near full power for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones:

Initiating Events, Mitigating Systems, and Barrier Integrity 1 R01 Adverse Weather Protection (71111.01 -1 sample) Impending Adverse Weather

a. Inspection Scope

Because severe weather was forecast in the vicinity of the facility for July 14, 2010, the Inspectors reviewed Entergy's overall preparations/protection for the expected weather conditions.

The inspectors walked down systems required for normal operation and shutdown conditions because their safety related functions could be affected, or required, as a result of high wind impacts or the loss of offsite power. The inspectors evaluated the plant staff's preparations in accordance with site procedures to determine if actions were adequate.

During the inspection, the inspectors focused on plant specific design features and station procedures used to respond to adverse weather conditions.

The inspectors also toured the site to identify loose debris that could become projectiles during a tornado. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant. Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for the systems selected for inspection, and reviewed whether operator actions were appropriate as specified by plant specific procedures.

The inspectors also reviewed a sample of corrective action program (CAP) items to verify that the licensee identified adverse weather impact issues at an appropriate threshold and dispositioned them through the CAP in accordance with station corrective action procedures.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

.1 1 Equipment

Alignment Partial System Walkdowns (71111.04Q -3 samples)

a. Inspection Scope

The inspectors performed partial system walkdowns of the follOwing risk significant systems: July 27,2010,22 safety injection train after post maintenance testing (PMT); September 14, 2010, 22 residual heat removal train after a maintenance outage; and September 27,2010,22 auxiliary feedwater (AFW) pump after a maintenance outage. The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected.

The inspectors focused on those conditions that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, technical specification requirements, technical specifications (TSs), work orders (WOs), condition reports (CRs), and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions.

The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.

The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no deficiencies.

The inspectors also reviewed whether Entergy staff had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three partial system walkdown samples as defined in NRC Inspection Procedure 71111.04.

b. Findings

No findings were identified . . Full System Walkdown (71111.04S -1 sample)

a. Inspection Scope

On September 21 and 22, 2010, the inspectors perfonmed a complete system alignment inspection of the safety injection system to verify the functional capability of the system. The inspectors selected this system because it was considered both safety significant and risk significant in the licensee's probabilistic risk assessment.

The inspectors inspected the system to review mechanical and electrical equipment line ups, electrical power availability, component lubrication and equipment cooling, hanger and support Enclosure

.1 functionality, operability

of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation.

In addition, the inspectors reviewed the CAP database to ensure that system adverse conditions were being identified and appropriately resolved.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as defined in NRC Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1 R05 Fire Protection Resident Inspector Quarterly Walkdowns (71111.05Q -5 samples)

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition offirefighting equipment in the following risk significant plant areas:

  • Pre-Fire Plan (PFP) 160A;
  • PFP-259. The inspectors reviewed areas to assess if Entergy personnel implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the station's fire plan. The inspectors selected fire areas based on their overall contribution to intemal fire risk and their potential to affect equipment that could initiate or mitigate a plant transient.

Using the documents listed in the attachment, the inspectors reviewed whether fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The inspectors also reviewed whether issues identified during the inspection were entered into the licensee's CAP. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five quarterly fire protection inspection samples as defined in NRC Inspection Procedure 71111.05.

b. Findings

No findings were identified . . 2 Annual Fire Drill (71111.05A

-1 sample)

a. Inspection Scope

On August 11, 2010, the inspectors observed a fire brigade activation involving a simulated fire in the vicinity of the hydrazine cylinders, which is located in the turbine building.

The observation involved an evaluation of the readiness of the plant fire brigade to fight fires. The inspectors reviewed whether Entergy staff identified performance deficiencies; openly discussed them in a critical manner at the drill debrief; and identified appropriate corrective actions. Specific attributes evaluated by the inspectors were (1) proper wearing of turnout gear and self contained breathing apparatus; (2) proper use and layout of fire hoses; (3) employment of appropriate fire fighting techniques; (4) sufficient firefighting equipment brought to the scene; (5) effectiveness of fire brigade leader communications, command, and control; (6) search for victims and propagation of the fire into other plant areas; (7) smoke removal operations; (8) utilization of preplanned strategies; (9) adherence to the preplanned drill scenario; and (10) drill objectives.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one annual fire protection inspection sample as defined in NRC Inspection Procedure 71111.05.<

b. Findings

No findings were identified.

1 R06 Flood Protection Measures (71111.06 -1 sample) Intemal Flooding Review

a. Inspection Scope

The inspectors reviewed the UFSAR, the site flooding analysis, and plant procedures to assess susceptibilities involving internal flooding; and reviewed the CAP to determine if the licensee identified and corrected flooding problems, and to verify whether operator actions for coping with flooding are adequate.

The inspectors also focused on the component cooling water pump room areas to verify the adequacy of equipment seals located below the flood line, floor and wall penetration seals, watertight door seals, common drain lines and sumps, sump pumps, level alarms, and control circuits, and temporary or removable flood barriers.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one internal flood protection measures inspection sample as defined in NRC Inspection Procedure 71111.06.

b. Findings

No findings were identified.

1Licensed Operator Requalification Program (71111.11 Q -1 sample) Quarterly Review

a. Inspection Scope

On September 1, 2010, the inspectors observed a crew of licensed operators, responding to a simulated event involving a steam generator tube rupture coincident with a loss of offsite power and the failure of select components to automatically start as required.

The inspectors observed the scenario in the plant's simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and that training was being conducted in accordance with licensee procedures.

The inspectors evaluated the following areas regarding crew and operator performance: Clarity and formality of communications; Implementation of timely actions; Prioritization, evaluation, and verification of annunciator alarms; Usage and implementation of abnormal and emergency procedures; Control board operations; . Identification and implementation of TS actions and emergency plan actions and notifications; and Oversight and direction from control room supervisors.

The inspectors compared the crew's performance in these areas to critical task completion reqUirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly licensed operator requalification program sample as defined in NRC Inspection Procedure 71111.11.

b. Findings

No findings were identified. 1 R Maintenance Effectiveness (71111.12Q -1 sample)

a. Inspection Scope

The inspectors reviewed the 22 static inverter to assess the effectiveness of maintenance activities on system performance and reliability.

The inspectors reviewed, when applicable, system health reports, corrective action program documents, maintenance work orders, and maintenance rule basis documents to ensure performance problems were being identified and properly evaluated within the scope of the maintenance rule. For each sample selected, the inspectors reviewed whether the Enclosure structure, system, and component (SSG) was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and reviewed whether the (a)(2) performance criteria established by Entergy staff was reasonable.

For SSCs classified as (a)(1), the inspectors assessed the adequacy of goals and corrective actions to return these SSCs to (a)(2). Additionally, the inspectors determined if Entergy staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one quarterly maintenance effectiveness sample as defined in NRC Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1 Maintenance Risk Assessments and Emergent Work Control (71111.13

-5 samples)

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the maintenance and emergent work activities affecting risk significant and safety related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work: July 19,2010, elevated risk due to severe weather with 22 fuel oil transfer pump out of service for planned testing; and 22 charging pump, 22 instrument air dryer, and feeder 96951 out of service for emergent maintenance; July 28,2010, elevated risk due to 23 charging pump out of service for planned maintenance and 6.9kV relay functional testing; August 19, 2010, elevated risk for 480 volt degraded voltage function and emergency diesel generator (EDG) out of service for planned calibration and testing of 480 volt undervoltage alarms; August, 24, 2010, elevated risk for 21 AFW pump test, and alternate safe shutdown supply breaker to 21 AFW pump test, during emergent maintenance on individual rod position indication D-8; and September 16,2010, elevated risk due to 21 EDG, refueling water storage tank level indicator, and residual heat removal valve 884 out of service for planned maintenance; and 21 service water pump out of service for emergent maintenance.

The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones.

As applicable for each activity, the inspectors verified that Entergy personnel performed risk assessments as required by 10 CFR 50.65{a)(4)and that the assessments were accurate and complete.

When Entergy personnel performed emergent work, the inspectors verified that operations personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the station's probabilistic risk analyst or shift technical advisor, to verify plant conditions were consistent with the risk Enclosure assessment.

The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of five maintenance risk and emergent work control inspection sample as defined in NRC Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1 R15 Operability Evaluations (71111.15 3 samples)

a. Inspection Scope

The inspectors reviewed the following issues:

  • July, 6, 2010, 480 volt switchgear room high temperature alarm;
  • July 20, 2010, EDG starting air capacity; and
  • August 17, 2010, EDG fuel oil leaks. The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred.

The inspectors compared the operability and design criteria in the appropriate sections of the TSs and UFSAR to Entergy's evaluations to determine whether the components or systems were operable.

Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled.

The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.

Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three operability evaluations inspection samples as defined in NRC Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1 R Plant Modifications (71111

.18 -1 sample) Temporary

Modifications

a. Inspection Scope

The inspectors reviewed the following temporary modification to verify that the safety functions of affected safety systems were not degraded:

On July 28, 2010, Entergy staff implemented Engineering Change (EC) 23681 in response to high upper thrust bearing temperatures on the 21 RCP motor. The temporary modification raised the upper thrust bearing temperature alarm setpoint from 185F to 190F and the. manual trip setpoint from 200F to 205F. This temporary modification remained in place until repair of the 21 RCP motor was completed September 13, 2010. The inspectors reviewed the temporary modification and the associated safety evaluation screening against the system design bases documentation, including the UFSAR and the TSs, and verified that the modification did not adversely affect the system operability/availability.

The inspectors also reviewed whether the installation and restoration were consistent with the modification documents and that configuration control was adequate.

Additionally, the inspectors verified that the temporary modification was identified on control room drawings, appropriate tags were placed on the affected equipment, and Entergy personnel evaluated the combined effects on mitigating systems and the integrity of radiological barriers.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample for temporary plant modifications as defined in NRC Inspection Procedure 71111.18.

b. Findings

No findings were identified. 1 R Post Maintenance Testing (PMT) (71111.19

-7 samples)

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability: . July 5,2010, B reactor trip breaker (RTB) replacement; July 6, 2010, temperature average signal computer after summing amplifier repair; July 21,2010,22 charging pump after internal valve replacement; July 21, 2010, rod position indicators E13 and L 13 after replacement; August 25, 2010, pilot operated relief valve disconnect switches EDC 10 and 11 after maintenance; September 7, 2010, 22 steam generator level bistable LC 427 NB after replacement; and September 16, 2010, 21 EDG after maintenance outage. The inspectors selected these activities based upon the structure, system, or component's ability to affect risk. The inspectors evaluated these activities to determine (as applicable)the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; and that test instrumentation was appropriate.

The inspectors evaluated the activities against the TSs, the UFSAR, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements.

In addition, the inspectors reviewed corrective action documents associated with PMTs to determine whether Entergy personnel were identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of seven PMT inspection samples as defined in NRC Inspection Procedure 71111.19.

b. Findings

Reactor Trip Breaker (RTB) Preventative Maintenance Procedure was not Adequately Implemented

Introduction:

A self-revealing Green NCV of 10 CFR 50, Appendix B, Criterion V "Instructions, Procedures and Drawings," was identified because Entergy staff did not adequately implement the PM procedure for the B RTB in March 2009.

Description:

On July 5,2010, control room operators observed the B RTB red indicating breaker closed lights were extinguished.

The red indicating breaker closed lights are in series with the shunt trip device and provide indication in the control room that the breaker trip mechanism is functioning properly.

After troubleshooting was conducted, Entergy operators determined the shunt trip device function was inoperable, entered the applicable TS action statement TS 3.3.1, "Reactor Protection System (RPS) Instrumentation," and issued CR-IP2-2010-4451.

The associated bypass breaker was racked in and the B RTB and its associated fuse block were replaced.

The B RTB shunt trip device was restored to operability in the timeframe provided in the TS action statement.

Entergy personnel generated was to replace fuse block assemblies for the remaining reactor trip and bypass breakers at the site. Indian Point Unit 2 has two reactor trip breakers in service that are normally closed during normal plant operations and two bypass breakers in parallel to each RTB for performing PM. The breakers have two tripping mechanisms which include the undervoltage coil and the shunt trip device. The tripping mechanisms serve to open the RTB when the RPS automatic trip logic is made up to interrupt power to the control rod drive mechanisms, which allows the shutdown and control rods to fall into the core by Enclosure i

gravity. The shunt trip device serves a redundant function that ensures the breaker opens if the undervoltage coil failed to function properly.

Entergy personnel performed an apparent cause evaluation (ACE) of the B RTB failure and determined that the B RTB red indicating lights in the control room were extinguished due to a degraded control power fuse holder. This degradation included a broken corner of the insulating material, loose fuse clips, exposed copper due to worn silver coating on contact points, distorted fuse Clip blades and poor contact resistance checks. The fuse holder when installed into the fuse case had insufficient tension and could be easily removed or installed without requiring significant force. Entergy personnel determined the degraded condition was due to a lack of questioning attitude and attention to detail by maintenance personnel during past PM inspections.

Entergy's ACE noted that the degraded condition developed over the course of several years and was evident at a minimum during the March 10,2009 performance of PM Procedure 0-BRK-401-ELC "Westinghouse, Reactor Trip and Bypass Circuit Breaker (DB-50)," which includes a step for checking the fuse holder. Entergy's corrective actions included:

reinforce conduct of maintenance in regards to activities of plant equipment within the maintenance and operations departments; enhance guidance for fuse block inspection in PM procedures; and evaluate the need for maintenance and operations department training enhancements associated with fuses and fuse block inspections.

The inspectors reviewed the ACE and completed PM procedure, and also identified that maintenance personnel identified issues with the control power fuses and a chip on the fuse holder; however, the adverse conditions were not communicated to the responsible engineer as required by Step 4.2.7 "Notify Responsible Engineer AND Supervisor of unusual conditions AND record below." In addition, a CR was not issued in accordance with the PM procedure and station standards.

The inspectors noted that Step 3.10 of the PM procedure states that "All unacceptable components and conditions SHALL be documented on Attachment 1 and Unacceptable Component Tracking Sheet accepted or corrected under the direction of the Component Engineer;" however, the attachment was not completed.

The inspectors also identified a separate issue with the procedure where maintenance personnel did not perform cell switch inspection and lubrication as required by Step 4.2.9. This step is necessary to ensure that the cell switches reset to their shelf position upon removal of a RTB and the reactor protection circuitry is established as designed.

Entergy personnel documented this issue in CR-IP2-201 0-5317 and performed Step 4.2.9 of the procedure during a forced outage in September 2010 under WO 249229 and did not identify an adverse condition.

Entergy's corrective actions included reviewing a sample of work packages under CR-IP3-201 0-1 022 to ensure all work packages were fully completed.

Analysis:

The performance deficiency associated with this finding was that Entergy personnel did not adequately implement the PM procedure for the B RTB in March 2009. This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems cornerstone and affects the cornerstone objective of ensuring the availability and reliability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, an inadequate PM implementation contributed to the failure of the shunt trip device function of the B RTB. Using IMC 0609.04, "Phase 1 -Initial Screening and Characterization of Findings," the finding was determined to have very low safety significance (Green) because the finding Enclosure did not result in a loss of system safety function because the undervoltage coil was operable; there was not an actual loss of safety function of a single train for greater than its technical specification allowed outage time; and the issue was not potentially risk significant due to a seismic, flooding, or severe weather initiating event. The finding has a cross-cutting aspect in the area of problem identification and resolution associated with the corrective action program attribute of complete and accurate identification of issues. Specifically, Entergy staff did not identify and communicate RTB conditions completely and accurately such that the B RTB conditions were fully identified in the CAP. [P.1.(a) per IMC 0310]

Enforcement:

10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures and Drawings," requires, in part, that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances and shall be accomplished in accordance with these procedures.

Contrary to the above, on March 10,2009, maintenance personnel did not adequately implement PM Procedure 0-BRK-401-ELC "Westinghouse, Reactor Trip and Bypass Circuit Breaker (DB-50)" which resulted in the inoperability of the B RTB shunt trip device on July 5, 2010. Entergy personnel took immediate corrective actions to replace the B RTB and its associated fuse block assembly.

Because this violation was of very low safety significance and it was entered into Entergy's CAP as CR-IP2-201 0-4451, this violation is being treated as a NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy: NCV 500024712010004-01, Reactor Trip Breaker Preventative Maintenance Procedure was not Adequately Implemented. 1 Refueling and Outage Activities (71111.20

-1 sample)

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Unit 2 planned maintenance outage to repair the 21 RCP, conducted September 3 -15, 2010. The inspectors' review considered whether Entergy personnel appropriately considered risk, industry experience, and previous site performance in developing and implementing a plan that assured maintenance of defense in depth with regards to reactor safety. During the maintenance outage, the inspectors observed portions of the shutdown and cooldown processes and monitored Entergy operator controls over the outage activities listed below: Configuration management, including maintenance of defense in depth, is commensurate with the outage safety plan for key safety functions and compliance with the applicable TSs when taking equipment out of service; Clearance activities, including confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing; Status and configuration of electrical systems to ensure that TSs and outage planning requirements were met, and controls over switchyard activities were appropriate; Monitoring of decay heat removal processes, systems. and components; Controls over activities that could affect reactivity; Maintenance of secondary containment as required by the TS; Enclosure Startup and ascension to full power operation, tracking of startup prerequisites, and walkdown of containment to verify that debris had not been left which could impact emergency core cooling system suction strainers; Station personnel identification and resolution of problems related to maintenance outage activities; and Work hours for fatigue concerns.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one other outage inspection sample as defined in NRC Inspection Procedure 71111.20.

b. Findings

No findings of significance were identified. Surveillance Testing (71111.22

-4 samples)

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems, and components, to assess whether test results satisfied Technical Specifications, UFSAR, technical requirements manual, and Entergy procedure requirements.

The inspectors verified that: test acceptance criteria were sufficiently clear; tests demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had accurate calibrations and appropriate range and accuracy for the application; tests were performed as written; and applicable test prerequisites were satisfied.

Following the tests, the inspectors considered Whether the test results supported conclusions that equipment was capable of performing the required safety functions.

The following surveillance tests were reviewed: June 30, 2010, 2-PT-Q62, high steam flow and turbine first stage pressure bistables test; July 30,2010, 2-PT-Q088, inservice testing of component cooling water check valves 790, 791. 798 &796. 793; August 4,2010, 2-PT-Q58, steam generator level bistables test; and August 19, 2010, 2-PT-M048, 480V undervoltage alarm test. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four surveillance testing inspection samples as defined in NRC Inspection Procedure 71111.22.

b. Findings

No findings were identified.

.1 Cornerstone:

Emergency Preparedness 1 EP6 Drill Evaluation (71114.06

-1 sample) Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of a routine Entergy emergency drill on September 1, 2010, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities.

The inspectors observed emergency response operations in the simulator to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures.

The inspectors also attended the station drill critique to compare inspector observations with those identified by Entergy staff in order to evaluate Entergy's critique and to verify whether the Entergy staff was properly identifying weaknesses and entering them into the CAP. Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in NRC Inspection Procedure 71114.06.

b. Findings

No findings were identified.

OTHER ACTIVITIES

40A 1 Performance Indicator Verification (71151 -2 samples) Mitigating Systems Performance Index -High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors sampled Entergy submittals for the mitigating systems performance index -high pressure injection systems PI for the period from July 2009 through June 2010. To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in Nuclear Energy Institute (NEt) Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed Entergy's operator narrative logs, issue reports, mitigating systems performance index derivation reports, event reports, and NRC integrated inspection reports to validate the accuracy of the submittals.

The inspectors also reviewed Entergy's issue report database to determine if problems had been identified with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the attachment to this report. These activities constitute completion of one mitigating systems performance index -high pressure injection system sample as defined in NRC Inspection Procedure 71151. Enclosure

===.1

b. Findings

No findings were identified . . 2 Mitigating===

Systems Performance Index -Heat Removal System (MS08)

a. Inspection Scope

The inspectors sampled Entergy submittals for the mitigating systems performance index -heat removal system PI for the period from July 2009 through June 2010. To determine the accuracy of the PI data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports, mitigating systems performance index derivation reports, and NRC integrated inspection reports to validate the accuracy of the submittals.

The inspectors also reviewed Entergy's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the attachment to this report. These activities constitute completion of one mitigating systems performance index -heat removal system sample as defined in NRC Inspection Procedure 71151.

b. Findings

No findings were identified.

40A2 Identification and Resolution of Problems (71152 -2 samples) Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, "Identification and Resolution of Problems," the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that issues were being entered into Entergy's CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed.

In order to assist with the identification of repetitive equipment failures and specific human performance issues for fOllOW-Up, the inspectors performed a daily screening of items entered into the CAP. The inspectors reviewed attributes that included:

(1) complete and accurate identification of the problem; (2) timely correction, commensurate with the safety significance; (3) evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and (4) classification, prioritization, focus, and timeliness of corrective actions. These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter. Specific documents reviewed during this inspection are listed in the attachment.

b. Findings

No findings were identified . . 2 Annual Sample -Review of Nonfunctional Emergency Light EL-6

a. Inspection Scope

The inspectors selected for review 0-5037 to determine if problems were being properly identified, characterized, and entered into the CAP for evaluation and resolution.

This documented a failure of Emergency Light (EL) EL-6 due to its light beams being misaligned during the last functional test. Entergy performed an extent of condition review with no issues identified.

The inspectors also conducted walkdowns and interviewed plant personnel to verify proper EL alignment.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one in-depth problem identification and resolution sample as defined in NRC Inspection Procedure 71152.

b. Findings and Observations

No findings were identified.

The inspectors identified the issue documented in CR-IP2-2010-5037 during a plant walkdown.

The inspectors reviewed the last completed Procedure 2-PT-M49A1B "Appendix R Emergency Lighting," and found that EL-6 had electrolyte added to its internal battery. Access to the battery is through the top cover, where the light beams are attached, and manipulating the top cover easily moves the light beams out of position.

The inspectors determined that the procedure checks the alignment of the light beams before adding electrolyte to the battery, but does not verify the light beams are in the correct position once the cover and lights are re-instal/ed.

This issue was entered into the licensee's CAP as CR-IP3-201 0-2576. The inspectors determined this issue is minor because the light found out of position was only used for access and egress paths; operations personnel carry flashlights when responding to fires; there was no impact on the operation of a safety related component; and no other light beams were found out of position over the last year. The inspectors determined that Entergy's corrective action to revise the functional test procedure to verify light beam alignment upon completion of the procedure is adequate . . 3 Annual Sample -Buried Pipe Inspection and Monitoring Program

a. Inspection Scope

The inspectors interviewed the Program Owner (Responsible Engineer)for the Indian Point Buried Pipe Inspection and Monitoring Program and reviewed the related applicable procedures for the program. The inspectors used as a reference the Electric Power Research Institute (EPRI) and NEI guidelines for buried pipe systems. Field observations were made of the areas of past and current buried pipe activities.

These included the Unit 2 and Unit 3 condensate storage tank (CST) and auxiliary feedwater

.1 19 (AFW) piping, and the piping exiting the Unit 3 reactor water storage tank to under the independent

spent fuel storage installation (ISFSI) haul path. The inspection scope included determining the status of site activities and plans to monitor and inspect buried piping and storage tanks. The inspectors ensured these activities met or exceeded the EPRI and NEI guidance and requirements to understand the condition of these components to minimize the occurrence of leakage. SpeCific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one in-depth problem identification and resolution sample, as defined in NRC Inspection Procedure 71152.

b. Findings and Observations

No findings were identified.

A leak in the Unit 2 AFW system 8-inch diameter return line to the CST was identified by Entergy staff on February 15,2009 and repaired.

In September 2009, guided wave inspection conducted by station personnel identified Level 2 G-scan indications in both the Unit 2 and Unit 3 AFW CST 12-inch diameter suction lines. Level 2 G-scan indications are areas of moderate interest where follow-up is recommended.

Entergy entered this condition for evaluation into the CAP as CR-IP2-2009-00666.

40A3 Event Follow-up (71153 -3 samples) (Closed) Licensee Event Report 05000247/2010-004-00, Plant Operation Outside Technical Specifications Due to a Leak in the Reactor Coolant Pressure Boundary.

a. Inspection Scope

On March 18, 2010, while Indian Point Unit 2 was shutdown for a refueling outage, Entergy staff identified boron accumulation at a socket weld from the reactor coolant pressure boundary on a three-quarter inch line located upstream of check valve 256B associated with 22 RCP seal bypass line. Based on visual inspections conducted by Entergy staff during its boric-acid walkdowns, Entergy personnel concluded that the leak most likely existed during plant operation based on the amount of dry boron accumUlation at the weld defect area. Entergy engineering personnel characterized the flaw as a rounded weld defect in the socket weld, which likely was introduced at the time of system construction and which propagated through-wall over time during plant operations as the result of service induced loading conditions.

Entergy maintenance technicians repaired the defect during the April 2010 outage. Entergy staff determined the leakage could have existed during plant operation and, therefore, the plant could have been operating contrary to TS 3.4.13, "RCS Operational Leakage," which limits operational pressure boundary leakage to zero. The inspectors reviewed the Licensee Event Report (LER), Entergy's evaluation of the event, and associated corrective actions contained in CR-I P2-20 1 0-01631. The inspectors determined that the weld defect and resultant leakage was not within Entergy's ability to foresee and correct based on review of Entergy's visual examination results, corrective action reviews and associated non-destructive examination requirements for this weld. This review was supplemented by inspector observations of this prior leakage condition observed by inspectors during the outage as part of NRC Inspection Procedure 71111.08.

Specifically, the inspectors affirmed that there were no in-service inspection requirements not implemented or previous corrective action information available to Entergy personnel that would have detected or reasonably indicated a weld defect for this particular socket weld. The inspectors also affirmed Entergy staff identified the leakage at the first reasonable opportunity.

Therefore, the inspectors concluded operation of Indian Point Unit 2 with RCS pressure boundary leakage is prohibited by TS 3.4.13. However, the inspectors determined that this weld defect could not have been avoided or detected by Entergy's quality assurance program or other related control measures, and did not constitute a performance deficiency.

These activities constitute completion of one event follow-up sample as defined in NRC Inspection Procedure 71153.

b. Findings

This issue is considered within the traditional enforcement process because there was no performance deficiency identified and NRC IMC 0612, Appendix B, "Issue Screening" directs disposition of this issue in accordance with the NRC Enforcement Policy. The inspectors used the Enforcement Policy, Section 6.1 -Reactor Operations, to evaluate the significance of this violation.

The inspectors concluded that the violation is more than minor and best characterized as Severity Level IV (very low safety Significance)because it is similar to Enforcement Policy Section 6.1, Example d.1. Additionally, the inspectors assessed the risk associated with the issue by using IMC 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations." The inspectors screened the issue and determined that RCS leakage is considered a Loss-of-Coolant Accident initiator, and evaluated using the Initiating Event criteria in Appendix A. Based on the weld defect size and characterization of the flaw, it is not expected this existing flaw would have impacted the structural integrity of the bypass line, the leakage would not result in exceeding the TS limit for identified RCS leakage (10 gpm) nor would the leakage have likely affected other mitigation systems resulting in a total loss of their safety function.

As a result, this issue would screen as very low safety significance (Green). Because this issue is of very low safety significance (Green) and it has been determined that this issue was not within Entergy's ability to foresee and correct, that Entergy staff's actions did not contribute to the degraded condition, and that actions taken were reasonable to identify and address this matter, and as such no performance deficiency exists, the NRC has decided to exercise enforcement discretion in accordance with Section 3.5 of the NRC Enforcement Policy and refrain from issuing enforcement action for the violation of TSs (EA-1 0-212). Further, because licensee actions did not contribute to this violation, it will not be considered in the assessment process or the NRC's Action Matrix. This LER is closed. Specific documents reviewed during this inspection are listed in the attachment.

.2 Loaded Multi-Purpose

Canister Stuck During Transfer from the HI-TRAC Transfer Cask to a H I-STORM Storage Cask

a. Inspection Scope

The inspectors reviewed the below listed equipment issue for plant status and mitigating actions to evaluate Entergy staff performance and confirm that Entergy staff implemented actions and notifications (if required)in accordance with station procedures.

From July through September, 2010, Entergy personnel conducted a campaign to place selected spent fuel elements into dry cask storage. On August 11, 2010, during the transfer of a fully loaded Multipurpose Canister (MPC) MPC-32 canister from the HI-TRAC transfer cask into a HI-STORM storage cask, the MPC became lodged while partially inserted into the HI-STORM cask. The MPC had been lowered approximately 18 inches into the H I-STORM from the H 1-TRAC, but became lodged and could not be lowered or raised with the fuel storage building (FSB) gantry crane. Through consultation with representatives of Holtec International (Holtec), the storage system vendor, Entergy personnel determined the problem to be a result of a mis-alignment of the HI-TRAC, the HI-STORM, and the mating device that joins the HI-TRAC to the HI-STORM for the MPC transfer.

After connections to the mating device and HI-TRAC were loosened, the FSB gantry crane main hOist was used to take up some of the HI-TRAC load. This manipulation freed up the MPC and it was able to be raised back into the HI-TRAC. The HI-TRAC and MPC were then lifted off the HI-STORM and mating device and placed into a safe storage position on August 13, 2010. Entergy personnel subsequently resumed dry cask operation during the week of August 16, 2010 and the MPC was able to be loaded into the HI-STORM on August 19.2010. The HI-STORM was subsequently placed on the ISFSI pad and no additional problems were encountered.

The inspectors reviewed Entergy actions and decision making to verify decisions were consistent with a conservative approach to assessing and addressing the condition.

The inspectors reviewed whether Entergy evaluations (and/or vendor supplied correspondence)were supported and addressed the thermal and structural performance of the MPC including a focus on the heat load of this loaded MPC to ensure the heat load remained below the Final Safety Analysis Report (FSAR) maximum permissible heat load limits. The inspectors also reviewed station evaluations that concluded that there was no structural damage to the air channels inside the HI-STORM and the thermal performance of the MPC and HI-STORM was not adversely affected.

These activities constitute completion of bne event follow-up sample as defined in NRC Inspection Procedure 71153.

b. Findings

No findings were identified.

The inspectors determined that Entergy and vendor-supplied evaluations appropriately concluded that the MPC was not adversely impacted in either thermal or structural performance.

Entergy entered the issue into the CAP and revised Holtec procedure 2-DCS-009-GEN, "MPC Transfer & HI-STORM Movement," to ensure that the mating device is properly aligned with the HI-STORM . . 3 Automatic Reactor Trip on High Steam Generator Water Level a. Inspection Scoge The inspectors reviewed the below listed event for plant status and mitigating actions to evaluate Entergy performance and confirm that Entergy operators implemented actions and notifications (if required)in accordance with station procedures.

The inspectors evaluated the response of control room personnel following the automatic reactor trip that occurred on September 3,2010, during a normal shutdown for a planned maintenance outage for repairs to the 21 reactor coolant pump motor. The Indian Point Unit 2 reactor automatically tripped from approximately 41% power in response to a main generator trip caused by high water level in the 23 steam generator.

The inspectors reviewed plant computer data, including the sequence of events report, evaluated plant parameter traces, and discussed the event with plant personnel, to verify that plant equipment responded as expected.

and to ensure that operating procedures were appropriately implemented.

The inspectors verified that operations personnel took appropriate actions in accordance with procedures in response to control rod H-8 indicating that the rod did not fully insert. The inspectors also verified that Entergy's post-trip review group (PTRG) identified the most probable cause(s) of the trip to facilitate corrective actions prior to restart. This event and the PTRG report were entered into Entergy's corrective action program as CR-IP2-2010-5484.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one event follow-up sample as defined in Inspection Procedure 71153.

b. Findings

No findings of Significance were identified.

The inspectors determined that operational response to the reactor trip was appropriate and that the indication problem with control rod H-8 was verified and corrected.

The inspectors will conduct further review of the root cause evaluation (RCE) and associated corrective actions in conjunction with review of the licensee event report to be submitted by Entergy personnel.

40A6 Meetings, Including Exit Exit Meeting Summary On October 28, 2010, the inspectors presented the inspection results of the integrated inspection to Mr. Joseph Pollock, Site Vice President, and other members of the Entergy staff. The licensee acknowledged the conclusions and observations presented.

The inspectors asked whether any materials examined during the inspection should be considered proprietary.

No proprietary information was identified.

ATTACHMENT:

=SUPPLEMENTAL

INFORMATION=

KEY POINTS OF CONTACT

Entergy Personnel

J. Pollock Site Vice President

R. Allen NDE Level III, Code Programs H. Anderson Specialist

-Nuclear Safety/Licensing

N.Azevedo

Supervisor

-Engineering

J. Baker Shift Manager M. Burney Specialist

-Nuclear Safety/Licensing

R. Burroni Manager -System Engineering

T. Cole Project Manager -NUC G. Dahl SpeCialist -Nuclear Safety/licensing

R. Daley Engineer III -Nuclear G. Dean Shift Manager D. Dewey Shift Manager G. Hocking Supervisor

-Radiation

Protection

R. Lee Buried Pipe and Tank Program Lead Engineer J. Lijoi Superintendent

-I&C L Lubrano Senior Lead Engineer R. Mages Senior HPfChemical

Specialist

T. McCaffrey

Manager -Design Engineering

T. Orlando Director, Engineering

S. Prussman Specialist

-Nuclear Safety/Licensing

J. Reynolds Corrective Action Specialist

T. Salentino

Superintendent

-Dry Fuel Storage S. Sandike Sr. HP/Chemical

Specialist

D. Smith Technical

Specialist

F. Spagnuolo

Supervisor

-Control Room M. Tesoriero

Manager -Programs and Components

A Vitale General Manager. Plant Operations

R. Walpole Manager, Licensing

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000247/2010-004-01 . NCV Reactor Trip Breaker Preventative

Maintenance

Procedure

was not Adequately

Implemented (Section 1 R19)

Closed

05000247/2010-004-00
LER Plant Operation
Outside Technical
Specifications
Due to a Leak in the Reactor Coolant Pressure Boundary (Section 40A3) Attachment

LIST OF DOCUMENTS

REVIEWED Common Documents Indian Point Unit 2 Control Room Narrative Indian Point Unit 2 Individual Plant Indian Point Unit 2 Individual Plant Examination of External Indian Point Unit 2 Plan of the Indian Point Unit 2 Technical Requirements Indian Point Unit 2 Technical Specifications and Indian Point Unit 2 Updated Final Safety Analysis Section 1 R01: Adverse Weather Protection

Procedures

2-AOP-FLOOD-1, Flooding, Rev. 6
IP-SMM, Event Notification and Reporting, Rev. 11
OAP-008, Severe Weather Preparations, Rev. 7 Condition Reports (CR-IP2-)
2010-04578

Miscellaneous

50.72 Event Notification
46092, July Individual Plant Examination for External Events for Indian Point Unit 2, Section Evaluation of Flood Area
PAS 68-1
IP-RPT-04-00230, Indian Point Unit 2 Probabilistic Safety Assessment, Rev. 1 Section 1 R04: Equipment Alignment

Procedures

2-ARP-SMF, CCR Safety Injection, Rev. 22 2-COL-4.2.1, Residual Heat Removal System. Rev. 27 2-COL-10.0, Locked Safeguards Valves. Rev. 40 2-COL-10.1.1, Safety Injection System, Rev. 33 2-COL-18.1, Main Steam and Reheat System, Rev. 38 2-COL-21.3, Steam Generator Water Level and Auxiliary Boiler Feedwater, Rev. 30 2-PT-2Y020A, 21 SICP Comprehensive Test, Rev. 1 2-S0P-1 0.1.1, Safety Injection Accumulators and Refueling Water Storage Tank Operations, Rev. 52
OAP-019, Component Verification and System Status Control. Rev. 5 Condition Reports (CR-IP2-)
2008-05043

Drawings

9321-F-2735, Safety Injection System, Rev. 140 Section 1 R05: Fire Protection

Procedures

IP2-RPT-03-00015, IP2 Fire Hazards Analysis, Rev. 2 Condition Reports (CR*IP2*)
2010-04515
2010*05048
2010-05075
Pre Fire Plan
PFP-160A, Appendix RlStation Black Out Emergency Diesel Generator Unit 1 -33'-0" Elevation, Rev.
PFP-205, Primary Auxiliary Building -35'*0" Elevation, Rev.
PFP-208, Primary Auxiliary Building -68'-0" Elevation, Rev.
PFP-209, Primary AUXiliary Building -68'-0" Elevation, Rev.
PFP-259, Auxiliary Feedwater Pump Room -18" Elevation, Rev. Miscellaneous
EN-DC-161, Control of Combustibles, Rev. 4 Section 1 ROG: Flood Protection Measures Procedures
2-AOP-FLOOO-1, Flooding, Rev. 6
OAP-008, Severe Weather Preparations, Rev. 7 Condition Reports (CR-IP2-)
2009-00456

Drawings

9321-F-2719-134, Waste Disposal System, April 14, 2006 Miscellaneous

Design Basis Document

for Component Cooling Water System, Rev. 1 Individual Plant Examination for External Events for Indian Point Unit 2, Section 5.2.2.1.3, Evaluation of Flood Area

PAB 68-1
IP-RPT-04-00230, Indian Point Unit 2 Probabilistic Safety Assessment, Rev. 1 UFSAR Section 11.1, Waste Disposal System, Rev. 21 Section 1 R11: Licensed Operator Requalification Program Procedures
2-E-3, Steam Generator Tube Rupture, Rev. 1 2-FR-S.1, Response to Nuclear Power Generation/Anticipated Transient Without SCRAM, Rev. 1
OAP-008, Severe Weather Preparations, Rev. 7 Attachment

Section 1R12: Maintenance

Effectiveness

Procedures

2-ARP-025.
Station Auxiliary Transformer, Rev. 1 Condition Reports
2008-01258
2008-02723
2008-02954
2009-00419
2009-01284
2010-02994
2010-03173

Work Orders

152061
234069
51324390
138 KV System Health Report, January -June, IPEC Combined Basis Document for 138 KV System, Rev. Operational Decision Making Instruction, Reactor Coolant Pump 21 Upper Oil Elevated Bearing Temperatures, June
29, Operations Narrative Logs -July 26, Reactor Coolant Pump 21 Upper Thrust Bearing Temperature Trend, June 23, September
2, 201 R&G Laboratories, Oil Analysis Severity for Reactor Coolant Pump 21, August 11, Section 1 R13: Maintenance Risk Assessments and Emergent Work Control Procedures
2-PT-M048, 480 Volt Undervoltage Alarm, Rev. 23 2-S0P 24.1.1, Service Water Hot Weather Operation, Rev. 11
EN-WM-104, On Line Risk Assessment, Rev. 1
IP-SMM-1 01, Online Risk Assessment, Rev. 3
OAP-008, Severe Weather Preparations, Rev. 6 Condition Reports (CR-IP2-)
2008-03893
2009-00154

Miscellaneous

Daily Status Report, Indian Point 2, August 24, 2010
DRN 10-4007, 2-PT-M048
Test Switch Monitor, Rev. 6 Operator Narrative Logs, July 19, 2010 Operator Narrative Logs, August 19, 2010 Operator Narrative Logs, August 24, 2010 Operator Narrative Logs, September
16,2010 Operator's Risk Report, July 19,2010 Operator's Risk Report, August 19, 2010 Operator's Risk Report, August 24, 2010 Operator's Risk Report, September
16, 2010 Technical Specification
3.3.5, Loss of Power Diesel Generator Start Instrumentation Technical Specification
3.8.1, AC Sources -Operating Updated Final Safety Analysis Report, Section 7.5.2.1.12, Bus Undervoltage, Rev. 21 Attachment

Section iRi5: Operability

Evaluations
2-ARP-SJF, Cooling Water and Air, Rev.
EN-OP-104, Operability Determination Process, Rev. Condition Reports
2006-07329
2010-04457
2010-04631'
2010-04711
2010-04753
2010-05173

Condition Reports

2006-04063
2008-00698
Work
247502
21-F-4017, Control Building Heating Vent and Air Conditioning, Rev.
GMH-00033-00, Indian Point 480V Switchgear Room Ventilation in the Event Some Dampers are Shut or in Closed Position, Rev.
IP-06-00329, Replacement of EDG Air Start Motors, Rev. Miscellaneous
2-ARP-003, Diesel Generator, Rev. 8 Emergency Diesel Generator Air Receiver Pressure Trends, July 2008 -July 2010 lO-lAR-2010-123, License Amendment Request for non-conservative technical specification
NRC Administrative letter 98-10, Dispositioning of Technical Specifications that are Insufficient to Assure Plant Safety NRC Inspection Manual, Part 9900: Technical Guidance, Operability Determinations and Functionality Assessments for Resolution of Degraded or Nonconforming Conditions Adverse to Quality or Safety, April 16, 2008 Technical Specification
3.8.3.F, Diesel Fuel Oil and Starting Air Standing Order 06-04, Non-Conservative Technical Specification
3.8.3.F

Section iRi8: Plant Modifications

Procedures

2-AOP-RCP-1, Reactor Coolant Pump Malfunction, Rev. 10 2-ARP-SCF, Condensate and Boiler Feed. Rev. 42
EN-DC-136, Temporary Modifications, Rev. 5
EN-LJ-100, Process Applicability Determination, Rev. 9 Condition Reports (CR-IP2-)
2010-04805
2010*04869

Work Orders

245127 Attachment

Miscellaneous

EC-23681, Raise 21 RCP Bearing Temperature Alarm Setpoint from 185F to 190F and Manual Trip Setpoint from 200F to 205

Section 1R19: Post-Maintenance

Testing
0-MS-412, Inspection and Cleaning of Bus Bars, Contacts, Ground Connections, Wiring Insulators, Rev. 2-PT-M21A, Emergency Diesel Generator Load Test, Rev. 2-PT-M7, Analog Rod Position Functional, Rev. 2-PT-W020, Electrical Verification

-Inverters and DC Distribution in Modes 1 to 4, Rev. 2-S0P-27.1.5, 480 Volt System, Rev.

EN-Ll-119, Apparent Cause Evaluation Process, Rev. Completed

Procedures

0-IC-SI-69, DAM502 Dual Alarm Module Replacement, Rev. 9, September
7, 2010 0-PMP-409-CVCS, Replacement of Fluid Cylinder Valves -Union
QX-300 Charging Pump, Rev. 2, July 21, 2010 0-PMP-413-CVCS, Inspection/Replacement of Charging Pump Fluid Cylinder Stuffing Box Seals, Rev. 2, July 21, 2010 2-PT-Q58, Steam Generator Level Bistables, Rev. 15, September
7,2010 Condition Reports (CR-IP2-)
2001-00908 2003-04862 2007-00577
2009-00010
2010-04451
2010-04453
2010-04557
2010-04699
2010-04720
2010-04816
2010-04864
2010-05163
2010-05208
2010-05317
2010-05399 2010-05698 2010-05772 2010-05776 2010-05790 2010-05795

Work Orders

174427
174427
2419
242655
242656
246479
51661337 Drawing 110E073, Reactor Breaker Schematic, Rev. 28 Miscellaneous Elgar Static Inverter Vendor Manual Emergency Diesel Generator Maintenance Outage Schedule, September
16, 2010 Technical Specification
3.1.7, Rod Position Indication Unit 2 -118V Instrument Bus System Health Report, 2 nd Qtr 2010 Section 1 R20: Refueling and Outage Activities

Procedures

2-POP-1.2, Reactor Startup, Rev. 54 2-POP-1.3, Plant Startup from Zero To 45% Power, Rev. 81 2-POP-2.1, Operation at Greater Than 45% Power, Rev. 57 Attachment
2-POP-3.1, Plant Shutdown from 45% Power, Rev. 2-POP-3.3, Plant Cooldown -Hot to Cold Shutdown, Rev. 2-PT-R156, Reactor Coolant System Boric Acid Leakage and Corrosion Inspection, Rev. 2-S0P-21.1, Main Feedwater System, Rev.
EM-OM-123, Fatigue management Program, Rev. Condition Reports
2010-05519 2010-05696
Work EmpCenter Fatigue Management Oil Analysis for 21 Reactor Coolant Pump, August 11, Operational Decision Making Instruction for 21 Reactor Coolant Pump, June 29, Outage Schedule for 21 Reactor Coolant Pump Repairs, July Trend for 21 Reactor Coolant Pump Bearing Temperatures, June 23 -September
3, Section 1 R22: Surveillance Testing Procedures
2-PT-M048, 480 Volt Undervoltage Alarm, Rev. 23 2-S0P-3.1, Charging, Seal Water, and Letdown Control, Rev. 66
EN-WM-104, Online Risk Assessment, Rev. 0 Completed

Procedures

2-PT-Q58, Steam Generator Level Bistables, Rev. 15, August 4,2010 2-PT-Q62, High Steam Flow and Turbine First Stage Pressure Bistables, Rev. 15, . June 30, 2010 2-PT-Q88, CCW Check Valve 790 and Stroke Testing of Valves 791, 798 & 796, 793, Rev. 6, July 30, 2010 Condition Reports (CR-IP2-)
2001-08968
2008-02231
2008-03893
2010-00846
2010-03430
2010-04365
2010-04888
2010-04928
2010-04952

Work Orders

52223773
52242119
253836 Calculation
FIX-000132, Steam Generator Narrow Range Instrument Loop Accuracy/SetpointiUncertainties, Rev. 0 Miscellaneous
DRN 10-4007, 2-PT-M048
Test Switch Monitor, Rev. 6 Operator Narrative Logs, August 19,2010 Operator's Risk Report, August 19, 2010 Attachment Technical Specification
3.3.5, loss of Power Diesel Generator Start Technical Specification
3.S.1, AC Sources -
Updated Final Safety Analysis Report, Section 7.5.2.1.12, Bus Undervoltage, Rev. Section 1 EP6: Drill Evaluation
IPEC-EP, Indian Point Emergency Plan, Rev. Condition Reports
2001-05584
2010-05444
2010-05445
2010-05461

Section 40A1: Performance

Indicator Verification
EN-Ll-114, Performance Indicator Process, Rev.
High Pressure Injection
PRA Model Update -January 10, Mitigating Systems Performance Indicator Basis Document, Rev. Mitigating Systems Performance Indicator Consolidated Data Entry Reports -High Injection, July 2009 -June 2010 Mitigating Systems Performance Indicator Consolidated Data Entry Reports -Residual Heat Removal, July 2009 -June 2010 Operator Narrative logs, July 2009 -June 2010 Residual Heat Removal PRA Model Update, January 10, 2008 System Health Reports -High Pressure Injection, July 2009 -June 2010 System Health Reports -Residual Heat Removal, July 2009 -June 2010

Section 40A2: Identification

and Resolution of Problems Procedures

CEP-BPT-0100, Buried Piping and Tanks Inspection and Monitoring, Rev. 0
EN-DC-167, Classification of Structures, Systems, and Components, Rev. 4
EN-DC-343, Buried Piping and Tanks Inspection and Monitoring Program, Rev. 2
EN-EP-S-002-MUl
TI, Buried Piping and Tanks General Visual Inspection, Rev. 0
EN-IS-112, Trenching, Excavating and Ground Penetrating Activities, Rev. 6 Entergy Buried PipinglTanks Action Plan, Rev. 3 IPEC Buried Piping and Tank Program Health Report for July 2009 -September
2009, as updated to July 6,2010 IPEC U2 and U3 Buried Pipe and Tank Inspections summary for October 12,2008 to March 31, 2010 IPEC U2 and U3 Safety Related and Rad fluid piping lists. Condition Reports
2008-04754
2009-00666
2010-00537

Condition Reports

400428. Appendix R Emergency Lighting Safe Shutdown Paths Emergency lighting Rev. Miscellaneous
EPRI Report
1016456, Recommendations for an Effective Program to Control the Degradation of Buried Inspection Report for AFW lines 1505. 1509 and 10" overflow, IPU2, December 4,
NEI 09-14, Guidance for the Management of Buried Piping Integrity, January Report
IP-RPT-09-00011, Corrosion
ICathodic Protection Field Survey and Assessment Underground Structures at IP U2 and U3. Rev. 0, October Root Cause Analysis Report for
CR-IP2-2009-00666, May SIA Report of G-Scan Assessment of various Buried pipe sections at IP U2 and September
23-24, 2009

Section 40A3: Event Follow-up

2-DCS-009-GEN, MPC Transfer &
HI-STORM Movement, Rev. 2-IC-PC-N-P-408A, Main Boiler Feed Pump Discharge Pressure Speed Control, Rev. 0 &
IP-EP-AD13, IPEC Emergency Plan Administrative Procedures, Rev.
IP-SMM-OP-105, Post Transient Evaluation, Rev. Completed

Procedures

2-PT-M49A, Appendix R Emergency Lighting (Conventional).
Rev. 22, August 3,2010 2-PT-M49B, Appendix R Emergency lighting (Nuclear), Rev. 14, August 3,2010 2-PT-R156, RCS Boric Acid Leakage and Corrosion Inspection, Rev. 1
IP-SMM-OP-105, Post Transient Evaluation, Rev. 6, September
3, 2010 Condition Reports (CR-IP2-) 2010-05082 2010-05484
2010-05487
2010-05494
2010-05496
2010-05587
2010-01631

Work Orders

182848-02

Miscellaneous

Engineering Correspondence, Inspection of Dry Cask Components Pertaining to Stuck MPC Condition, August 17, 2010 Entergy letter from Clay Wilson, IPEC System Engineering.

to Holtec International dated August 17,2010, Subject: Inspection of Dry Cask Components pertaining to stuck MPC condition, August 12. 2010 Holtec International letter to Tim Salentino, IPEC, Subject: Resumption of MPC transfer at IP2, August 18, 2010 Holtec International letter to Tim Salentino, IPEC, Subject: Structural and Thermal review of Stuck MPC condition at IP2, August 16,2010 Holtec Letter, Resumption of MPC Transfer at IP2, August 18, 2010 Holtec Letter, Structural and Thermal Review of Stuck MPC Condition at IP2, August 16, 2010 Attachment

IPEC Procedure Review and Approval Form
IP-SMM-AD-102, Rev. 6, for Procedure
MPC Transfer &
HI-STORM Movement, No. 2-DSC-009-GEN, Rev. 8 Operator Narrative Logs, September
3, 2010 Attachment
2R19 ACE ADAMS AFW CAP CFR CR CST EC EDG EL EPRI FSAR IMC ISFSI LER MPC NCV NEI NRC PFP PI PM PMT PTRG ,QP RCP RCS RCE RPS RTB SSC ST TS UFSAR URI WO A-11

LIST OF ACRONYMS

Spring 2010 refueling

outage Apparent Cause Evaluation

Agency Wide Document Management

System Auxiliary

Feedwater ,Corrective

Action Program Code of Federal Regulations

Condition

Report Condensate

Storage Tank Engineering

Change Emergency

Diesel Generator

Emergency

Light Electric Power Research Institute

Final Safety Analysis Report Inspection

Manual Chapter Independent

Spent Fuel Storage Installation

Licensee Event Report Multipurpose

Canister Non-Cited

Violation

Nuclear Energy Institute

Nuclear Regulatory

Commission

Pre-Fire Plan Performance

Indicator

Preventive

Maintenance

Post Maintenance

Test Post-trip

Review Group Augmented

Quality Reactor Coolant Pump Reactor Coolant System Root Cause Evaluation

Reactor Protection

System Reactor Trip Breaker Structures, Systems, and Components

Surveillance

Test Technical

Specifications

Updated Final Safety Analysis

Report Unresolved

Item Work Order Attachment