IR 05000416/2002004: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:October 24, 2002 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Entergy Operations, Inc. | Entergy Operations, Inc. | ||
-2-Should you have any questions concerning this inspection, we will be pleased to discuss them with you. | |||
Sincerely, | Sincerely, | ||
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P.O. Box 31995 Jackson, Mississippi 39286-1995 Wise, Carter, Child & Caraway P.O. Box 651 Jackson, Mississippi 39205 Winston & Strawn 1400 L Street, N.W. - 12th Floor Washington, DC 20005-3502 Director Division of Solid Waste Management Mississippi Department of Natural Resources P.O. Box 10385 Jackson, Mississippi 39209 President, District 1 Claiborne County Board of Supervisors P.O. Box 339 Port Gibson, Mississippi 39150 | P.O. Box 31995 Jackson, Mississippi 39286-1995 Wise, Carter, Child & Caraway P.O. Box 651 Jackson, Mississippi 39205 Winston & Strawn 1400 L Street, N.W. - 12th Floor Washington, DC 20005-3502 Director Division of Solid Waste Management Mississippi Department of Natural Resources P.O. Box 10385 Jackson, Mississippi 39209 President, District 1 Claiborne County Board of Supervisors P.O. Box 339 Port Gibson, Mississippi 39150 | ||
Entergy Operations, Inc. -3-General Manager Grand Gulf Nuclear Station Entergy Operations, Inc. | Entergy Operations, Inc. | ||
-3-General Manager Grand Gulf Nuclear Station Entergy Operations, Inc. | |||
P.O. Box 756 Port Gibson, Mississippi 39150 The Honorable Richard Ieyoub Attorney General Department of Justice State of Louisiana P.O. Box 94005 Baton Rouge, Louisiana 70804-9005 Office of the Governor State of Mississippi Jackson, Mississippi 39201 Mike Moore, Attorney General Frank Spencer, Asst. Attorney General State of Mississippi P.O. Box 22947 Jackson, Mississippi 39225 Dr. F. E. Thompson, Jr. | P.O. Box 756 Port Gibson, Mississippi 39150 The Honorable Richard Ieyoub Attorney General Department of Justice State of Louisiana P.O. Box 94005 Baton Rouge, Louisiana 70804-9005 Office of the Governor State of Mississippi Jackson, Mississippi 39201 Mike Moore, Attorney General Frank Spencer, Asst. Attorney General State of Mississippi P.O. Box 22947 Jackson, Mississippi 39225 Dr. F. E. Thompson, Jr. | ||
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P.O. Box 756 Port Gibson, Mississippi 39150 | P.O. Box 756 Port Gibson, Mississippi 39150 | ||
Entergy Operations, Inc. | Entergy Operations, Inc. | ||
-4-Electronic distribution by RIV: | |||
Regional Administrator (EWM) | Regional Administrator (EWM) | ||
DRP Director (KEB) | DRP Director (KEB) | ||
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GG Site Secretary (MJS) | GG Site Secretary (MJS) | ||
Dale Thatcher (DFT) | Dale Thatcher (DFT) | ||
R;\_GG\2002\GG2002-04RP-TLH.wpd RIV:RI:DRP/A SRI:DRP/A DRS/PSB DRS/EMB PE:DRP/A RWDeese | R;\\_GG\\2002\\GG2002-04RP-TLH.wpd RIV:RI:DRP/A SRI:DRP/A DRS/PSB DRS/EMB PE:DRP/A RWDeese TLHoeg DRCarter CSMarschall JMKeeton E-WDJohnson E-WDJohnson E-WDJohnson | ||
10/22/02 | /RA/ | ||
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10/22/02 | 10/22/02 10/22/02 10/22/02 10/23/02 10/22/02 SPE:DRP/A C:DRP/A CJPaulk WDJohnson | ||
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10/22/02 10/24/02 OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax | |||
ENCLOSURE U.S. NUCLEAR REGULATORY COMMISSION | ENCLOSURE U.S. NUCLEAR REGULATORY COMMISSION | ||
==REGION IV== | ==REGION IV== | ||
Docket: 50-416 License: NPF-29 Report No: 50-416/02-04 Licensee: Entergy Operations, Inc. | Docket: | ||
50-416 License: | |||
NPF-29 Report No: | |||
50-416/02-04 Licensee: | |||
Entergy Operations, Inc. | |||
Facility: Grand Gulf Nuclear Station Location: Waterloo Road Port Gibson, Mississippi 39150 Dates: June 30 through September 28, 2002 Inspectors: T. L. Hoeg, Senior Resident Inspector D. R. Carter, Health Physicist R. W. Deese, Resident Inspector J. M. Keeton, Project Engineer C. J. Paulk, Senior Project Engineer W. C. Sifre, Reactor Inspector Approved By: W. D. Johnson, Chief, Project Branch A Division of Reactor Projects Attachment: Supplemental Information | Facility: | ||
Grand Gulf Nuclear Station Location: | |||
Waterloo Road Port Gibson, Mississippi 39150 Dates: | |||
June 30 through September 28, 2002 Inspectors: | |||
T. L. Hoeg, Senior Resident Inspector D. R. Carter, Health Physicist R. W. Deese, Resident Inspector J. M. Keeton, Project Engineer C. J. Paulk, Senior Project Engineer W. C. Sifre, Reactor Inspector Approved By: | |||
W. D. Johnson, Chief, Project Branch A Division of Reactor Projects Attachment: | |||
Supplemental Information | |||
SUMMARY OF FINDINGS IR 05000416-02-04, Entergy Operations, Inc., on 6/30/02 - 09/28/02; Grand Gulf Nuclear Station. Postmaintenance testing, surveillance testing. | SUMMARY OF FINDINGS IR 05000416-02-04, Entergy Operations, Inc., on 6/30/02 - 09/28/02; Grand Gulf Nuclear Station. Postmaintenance testing, surveillance testing. | ||
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"Reactor Oversight Process," Revision 3, dated July 2000. | "Reactor Oversight Process," Revision 3, dated July 2000. | ||
A. Inspector Identified Findings Cornerstone: Mitigating Systems | A. | ||
* Green. The licensee failed to establish appropriate instructions for the circumstances when backfilling the reactor core isolation cooling high steam flow transmitter. This resulted in technicians improperly backfilling the detector. This caused the detector to isolate steam to the reactor core isolation cooling turbine, rendering the system inoperable. | |||
Inspector Identified Findings Cornerstone: Mitigating Systems | |||
* | |||
Green. The licensee failed to establish appropriate instructions for the circumstances when backfilling the reactor core isolation cooling high steam flow transmitter. This resulted in technicians improperly backfilling the detector. This caused the detector to isolate steam to the reactor core isolation cooling turbine, rendering the system inoperable. | |||
This violation of Technical Specification 5.4.1 is noncited in accordance with Section VI.A of the NRC's Enforcement Policy, and is in the licensee's corrective action program (CR-GGN-2002-0947). The finding was of very low safety significance because although the reactor core isolation cooling system was inoperable, all other remaining mitigating systems remained operable and the duration of the system inoperability was short (Section 1R19). | This violation of Technical Specification 5.4.1 is noncited in accordance with Section VI.A of the NRC's Enforcement Policy, and is in the licensee's corrective action program (CR-GGN-2002-0947). The finding was of very low safety significance because although the reactor core isolation cooling system was inoperable, all other remaining mitigating systems remained operable and the duration of the system inoperability was short (Section 1R19). | ||
B. Licensee Identified Findings A violation of very low safety significance, which was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and its corrective action tracking number are listed in Section 4OA7 of this report. | B. | ||
Licensee Identified Findings A violation of very low safety significance, which was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and its corrective action tracking number are listed in Section 4OA7 of this report. | |||
Report Details Summary of Plant Status: The plant began the inspection period at 100 percent rated thermal power and subsequently performed a planned power reduction to 80 percent on June 30, 2002, for initial startup of the auxiliary cooling tower. The plant was then operated at or near 100 percent rated thermal power except for periodic planned power reductions for monthly control rod exercising and periodic control rod pattern adjustments until July 25, when a partial loss of radial well pumping capability necessitated a power reduction to 78 percent of rated power. Following the recovery of all radial wells, the plant returned to 100 percent power and remained there until August 5, when the plant began coasting down in power. The coastdown ended on September 13, with the plant at 84 percent rated thermal power when the plant entered a refueling outage. The plant remained shutdown in this outage for the remainder of the inspection period. | Report Details Summary of Plant Status: The plant began the inspection period at 100 percent rated thermal power and subsequently performed a planned power reduction to 80 percent on June 30, 2002, for initial startup of the auxiliary cooling tower. The plant was then operated at or near 100 percent rated thermal power except for periodic planned power reductions for monthly control rod exercising and periodic control rod pattern adjustments until July 25, when a partial loss of radial well pumping capability necessitated a power reduction to 78 percent of rated power. Following the recovery of all radial wells, the plant returned to 100 percent power and remained there until August 5, when the plant began coasting down in power. The coastdown ended on September 13, with the plant at 84 percent rated thermal power when the plant entered a refueling outage. The plant remained shutdown in this outage for the remainder of the inspection period. | ||
1. REACTOR SAFETY Initiating Events, Mitigating Systems, Barrier Integrity [Reactor - R] | 1. | ||
REACTOR SAFETY Initiating Events, Mitigating Systems, Barrier Integrity [Reactor - R] | |||
1R01 Adverse Weather Protection (71111.01) | 1R01 Adverse Weather Protection (71111.01) | ||
a. Inspection Scope The inspectors reviewed one sample of Grand Gulf Nuclear Station (GGNS) personnels protection of the three divisions of the 125 Volt dc engineered safety features (ESF) | a. | ||
batteries for sustained hot weather conditions since these components are housed in rooms that are ventilated but not air conditioned. This review included walkdowns of the battery rooms focusing on hot weather susceptibilities, reviews of the systems designed ventilation features, and a review of the licensees actions to ensure the batteries remain operable in hot weather. Technical Manual "C&D Station Battery Installation and Operating Instructions," dated October 12, 1995, was also reviewed to check the vendors recommendations for sustained battery operations at higher than the | |||
Inspection Scope The inspectors reviewed one sample of Grand Gulf Nuclear Station (GGNS) personnels protection of the three divisions of the 125 Volt dc engineered safety features (ESF) | |||
batteries for sustained hot weather conditions since these components are housed in rooms that are ventilated but not air conditioned. This review included walkdowns of the battery rooms focusing on hot weather susceptibilities, reviews of the systems designed ventilation features, and a review of the licensees actions to ensure the batteries remain operable in hot weather. Technical Manual "C&D Station Battery Installation and Operating Instructions," dated October 12, 1995, was also reviewed to check the vendors recommendations for sustained battery operations at higher than the 77 F reference temperature. | |||
b. | |||
Findings No findings of significance were identified. | |||
1R04 Equipment Alignment | 1R04 Equipment Alignment | ||
.1 Partial System Walkdowns (71111.04) | |||
a. Inspection Scope The inspectors performed partial system walkdown inspections and reviews of a train in each of three systems important to reactor safety in order to verify the operability of the systems. The inspectors reviewed system operating instructions, system valve and breaker lineups, operator logs, and control room indications. The inspectors also verified valves, breakers, and control circuits were in their required positions for operability. The following systems were inspected: | a. | ||
Inspection Scope The inspectors performed partial system walkdown inspections and reviews of a train in each of three systems important to reactor safety in order to verify the operability of the systems. The inspectors reviewed system operating instructions, system valve and breaker lineups, operator logs, and control room indications. The inspectors also verified valves, breakers, and control circuits were in their required positions for operability. The following systems were inspected: | |||
-2- | |||
* | |||
Emergency diesel generator, Division I | |||
* | |||
Low pressure core spray system | |||
* | |||
Standby service water system, Train A b. | |||
Findings No findings of significance were identified. | |||
.2 Semi-Annual Complete System Walkdown (71111.04S) | .2 Semi-Annual Complete System Walkdown (71111.04S) | ||
a. Inspection Scope During the week of July 22, 2002, the inspectors performed a complete walkdown of the Division II emergency diesel generator to determine if there were any discrepancies between the actual equipment alignment versus what was procedurally required. During the walkdown, System Operating Instruction 04-1-01-P75-1, "Standby Diesel Generator System," Revision 62, Surveillance Procedure 06-OP-1P75-V-0013, "Standby Diesel Generator (SDG) 12 Operability Verification," Revision 103, and Drawing M-1070B, | a. | ||
Inspection Scope During the week of July 22, 2002, the inspectors performed a complete walkdown of the Division II emergency diesel generator to determine if there were any discrepancies between the actual equipment alignment versus what was procedurally required. During the walkdown, System Operating Instruction 04-1-01-P75-1, "Standby Diesel Generator System," Revision 62, Surveillance Procedure 06-OP-1P75-V-0013, "Standby Diesel Generator (SDG) 12 Operability Verification," Revision 103, and Drawing M-1070B, | |||
"Standby Diesel Generator System," Revision 30, were used by the inspectors to verify major diesel generator components were correctly labeled and aligned. The inspectors also reviewed open condition reports on the system for any deficiencies that could affect the ability of the system to perform its design function. Documentation associated with control room deficiencies, temporary modifications, operator workarounds, and items tracked by plant engineering were also reviewed to assess their collective impact on system operation. | |||
b. Findings No findings of significance were identified. | b. | ||
Findings No findings of significance were identified. | |||
1R05 Fire Protection (71111.05) | 1R05 Fire Protection (71111.05) | ||
.1 Quarterly Tours (71111.05Q) | |||
a. | a. | ||
Inspection Scope The inspectors reviewed area fire plans and performed walkdowns of six plant areas to assess the materiel condition and operational status of fire detection, suppression systems and equipment; the materiel condition of fire barriers; and the control of transient combustibles. Specific risk-significant plant areas included: | |||
* | |||
Division III emergency diesel generator room, Room 1D304 | |||
* | |||
Division III switchgear room, Room 0C210 | |||
* | |||
Electrical penetration room, Room 1A318 | |||
* | |||
ESF Heating, ventilation, and air conditioning equipment room, Room 0C302 | |||
* | |||
Residual heat removal (RHR) Pump C Room 1A118 | |||
* | |||
Standby service water Pump B Room 2M110 | |||
-3-b. | |||
Findings No findings of significance were identified. | |||
.2 Annual Drill Observation (71111.05A) | .2 Annual Drill Observation (71111.05A) | ||
a. Inspection Scope On August 29, 2002, the inspectors observed a fire brigade drill staged in Room 0C403, computer and control panel room, to evaluate the readiness of the fire brigade to fight fires. The inspectors reviewed the strategies and information in Fire Preplan C-10, | a. | ||
Inspection Scope On August 29, 2002, the inspectors observed a fire brigade drill staged in Room 0C403, computer and control panel room, to evaluate the readiness of the fire brigade to fight fires. The inspectors reviewed the strategies and information in Fire Preplan C-10, | |||
"Computer and Control Panels, Room 0C403, Area 25A," Revision 11, to verify if it was consistent with the fire protection design features, fire area boundaries, and combustible loading assumptions shown in the fire protection plan. The inspectors observed the fire brigade members: (1) donning protective clothing, (2) selecting turnout gear, (3) entering the fire zone, (4) using the fire preplan strategies, and (5) communicating with the control room staff. The inspectors observed the fire fighting equipment brought to the fire scene to evaluate whether sufficient equipment was available for the simulated fire. The inspectors observed fire fighting directions and radio communications between the brigade leader, brigade members, and the control room. | |||
b. | |||
Findings No findings of significance were identified. | |||
1R06 Flood Protection (71111.06) | 1R06 Flood Protection (71111.06) | ||
.1 Internal Flooding a. | |||
Inspection Scope The inspectors reviewed one sample of the GGNSs internal flooding protection features associated with the general flood protection measures for RHR Pump C room. The inspectors also reviewed specific flood protection measures associated with Maintenance Action Item (MAI) 307083 for the cleaning of the auxiliary decay heat removal heat exchangers which are housed in the RHR Pump C room. In order to clean the heat exchangers, the flood door for the RHR Pump C room was propped open to facilitate the necessary equipment. The inspectors performed a walkdown of the area reviewing internal flooding vulnerabilities, questioned maintenance personnel on contingencies for having the door propped open, and reviewed the protective features and procedures for mitigating the impact of any flooding. | |||
b. | |||
Findings No findings of significance were identified. | |||
-4- | -4- | ||
.2 External Flooding a. | |||
Inspection Scope The inspectors reviewed the Technical Requirements Manual Specification 6.7.5 and performed visual inspections of Culvert Number 1, examining its blockage and slope. | |||
The inspectors also reviewed flood protection measures for external sources as described in the Updated Final Safety Analysis Report and Calculation C-A-254.5 | The inspectors also reviewed flood protection measures for external sources as described in the Updated Final Safety Analysis Report and Calculation C-A-254.5 | ||
"Evaluation of the Effect of Predictive Maximum Precipitation Flood Levels Above Elevation 133 Feet on Safe Plant Operation, Revision 1, and the associated Supplement 1, Revision 0, to that calculation, and then performed walkdowns to verify that the assumptions made in the external flooding analyses remained valid. | |||
b | b. | ||
1R08 Inservice Inspection Activities (71111.08) | Findings No findings of significance were identified. | ||
1R08 Inservice Inspection Activities (71111.08) | |||
.1 Performance of Nondestructive Examination (NDE) Activities a. | |||
Inspection Scope The inspector requested and reviewed the NDE records for work that was performed for the current outage at the Grand Gulf Nuclear Station. The inspector also observed the following ultrasonic and magnetic particle examinations: | |||
* | |||
C11-G1010-W30 Control Rod Drive System | |||
* | |||
E51-G004-W29 Reactor Core Isolation Coolant System The inspector reviewed two weld repairs and two indications that were accepted for continued service. They were performed in accordance with ASME Code requirements. | |||
The inspector reviewed licensee NDE and contractor personnel qualification and certification records to determine if the NDE personnel were certified to perform the above examinations. The inspector also reviewed ultrasonic calibration records to verify acceptability to ASME Code requirements. | The inspector reviewed licensee NDE and contractor personnel qualification and certification records to determine if the NDE personnel were certified to perform the above examinations. The inspector also reviewed ultrasonic calibration records to verify acceptability to ASME Code requirements. | ||
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The inspector reviewed the implementation of the containment inservice inspection program plan against the requirements of ASME Section XI, Subsection IWE. | The inspector reviewed the implementation of the containment inservice inspection program plan against the requirements of ASME Section XI, Subsection IWE. | ||
b. Findings No findings of significance were identified. | b. | ||
Findings No findings of significance were identified. | |||
-5- | -5- | ||
.2 Problem Identification and Resolution a. | |||
Inspection Scope The inspector performed a detailed review of a sample of condition reports initiated within the past 2 years in the area of inservice inspection activities. The review was conducted to ascertain that the plant personnel were identifying performance issues within the inservice inspection program. This review assessed the effectiveness of cause determination, corrective action, and the adequacy of the plant personnels effort to identify transportability and generic issues. The review also assessed the effectiveness of the plant personnels effort to identify and address programmatic issues within the inservice inspection program. | |||
b. Findings No findings of significance were identified. | b. | ||
Findings No findings of significance were identified. | |||
1R11 Licensed Operator Requalification (71111.11Q) | 1R11 Licensed Operator Requalification (71111.11Q) | ||
a | a. | ||
b. Findings No findings of significance were identified. | Inspection Scope On August 1, 2002, the inspectors observed one session of licensed operator requalification training activities in the simulator to assess the licensee's effectiveness in conducting the requalification program and to verify that licensed individuals received the appropriate level of training required to maintain their licenses. The observed training consisted of establishing shutdown cooling and other nonroutine activities in preparation for the refueling outage. The inspectors also observed the post-training critique conducted by the training instructor and the shift manager to verify that weak areas observed during simulator operations were appropriately identified for additional training. | ||
b. | |||
Findings No findings of significance were identified. | |||
1R12 Maintenance Rule Implementation (71111.12Q) | 1R12 Maintenance Rule Implementation (71111.12Q) | ||
a. Inspection Scope The inspectors reviewed performance-based problems involving three selected in-scope structures, systems, or components (SSCs) to assess the effectiveness of the Maintenance Rule Program. Reviews focused on: (1) proper Maintenance Rule scoping in accordance with 10 CFR 50.65; (2) characterization of failed SSCs; (3) safety significance classifications; (4) 10 CFR 50.65 (a)(1) and (a)(2) classifications; and, (5) the appropriateness of performance criteria for SSCs classified as (a)(2), and goals and corrective actions for SSCs classified as (a)(1). The inspectors reviewed the most recent system health reports and system functional failures for the last two years. The following conditions were reviewed: | a. | ||
Inspection Scope The inspectors reviewed performance-based problems involving three selected in-scope structures, systems, or components (SSCs) to assess the effectiveness of the Maintenance Rule Program. Reviews focused on: (1) proper Maintenance Rule scoping in accordance with 10 CFR 50.65; (2) characterization of failed SSCs; (3) safety significance classifications; (4) 10 CFR 50.65 (a)(1) and (a)(2) classifications; and, (5) the appropriateness of performance criteria for SSCs classified as (a)(2), and goals and corrective actions for SSCs classified as (a)(1). The inspectors reviewed the most recent system health reports and system functional failures for the last two years. The following conditions were reviewed: | |||
-6- | |||
* | |||
Containment Isolation Valve E12F044A inoperability | |||
* | |||
Control rod drive system failures for Control Rods 12-13 and 60-37 | |||
* | |||
Control room air conditioning Train B operational failures b. | |||
Findings No findings of significance were identified. | |||
1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13) | 1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13) | ||
a. Inspection Scope Throughout the inspection period, the inspectors reviewed weekly and daily work schedules to determine when risk-significant activities were scheduled. The inspectors discussed five selected activities with operations and work control personnel regarding risk evaluations and overall plant configuration control. The inspectors discussed emergent work issues with work control center personnel and reviewed the prioritization of scheduled activities. The inspectors verified the performance of plant risk assessments related to planned and emergent maintenance activities as required by 10 CFR 50.65(a)(4) and Plant Procedure 01-S-18-6, "Risk Assessment of Maintenance Activities," Revision 1. | a. | ||
Inspection Scope Throughout the inspection period, the inspectors reviewed weekly and daily work schedules to determine when risk-significant activities were scheduled. The inspectors discussed five selected activities with operations and work control personnel regarding risk evaluations and overall plant configuration control. The inspectors discussed emergent work issues with work control center personnel and reviewed the prioritization of scheduled activities. The inspectors verified the performance of plant risk assessments related to planned and emergent maintenance activities as required by 10 CFR 50.65(a)(4) and Plant Procedure 01-S-18-6, "Risk Assessment of Maintenance Activities," Revision 1. | |||
Specific maintenance items reviewed during this period included: | Specific maintenance items reviewed during this period included: | ||
* | |||
MAI 297570, Hydrogen Recombiner B | |||
* | |||
MAI 307035, Low pressure core spray system | |||
* | |||
MAI 315778, Train B suppression pool makeup system | |||
* | |||
MAI 316476, Train A RHR system | |||
* | |||
MAI 318122, Instrument air system b. | |||
Findings No findings of significance were identified. | |||
1R14 Personnel Performance During Nonroutine Events (71111.14) | 1R14 Personnel Performance During Nonroutine Events (71111.14) | ||
.1 Loss of Spent Fuel Pool Cooling a. Inspection Scope On August 22, 2002, the plant experienced a loss of spent fuel pool cooling. The leak detection system (LDS) isolated and secured the fuel pool cooling and clean-up system when the LDS standpipe did not drain quickly enough after water was drained into the standpipe following restoration of a maintenance lineup. GGNS personnel investigated and discovered that the standpipe drain line was blocked and not allowing the standpipe to drain. The standpipe sensed this high level for an extended time and LDS logic interpreted this as a leak that the drain line could not keep up with and by design secured the running spent fuel pool cooling pump. GGNS personnel were able to assess the cause of the pump securing and restore fuel pool cooling in 44 minutes | .1 Loss of Spent Fuel Pool Cooling a. | ||
Inspection Scope On August 22, 2002, the plant experienced a loss of spent fuel pool cooling. The leak detection system (LDS) isolated and secured the fuel pool cooling and clean-up system when the LDS standpipe did not drain quickly enough after water was drained into the standpipe following restoration of a maintenance lineup. GGNS personnel investigated and discovered that the standpipe drain line was blocked and not allowing the standpipe to drain. The standpipe sensed this high level for an extended time and LDS logic interpreted this as a leak that the drain line could not keep up with and by design secured the running spent fuel pool cooling pump. GGNS personnel were able to assess the cause of the pump securing and restore fuel pool cooling in 44 minutes | |||
-7-without any noticeable rise in fuel pool temperature. The inspectors responded to the plant and observed the recovery lineup of the fuel pool cooling system. The inspector reviewed Off-Normal Event Procedure 05-1-02-III-1, "Inadequate Decay Heat Removal," | |||
Revision 24, along with GGNS personnels actions for procedural compliance. The inspectors also reviewed licensee actions with regard to 10 CFR 50.72 and 10 CFR 50.73 reporting requirements. Licensee actions were documented in Condition Report CR-GGN-2002-1575. | Revision 24, along with GGNS personnels actions for procedural compliance. The inspectors also reviewed licensee actions with regard to 10 CFR 50.72 and 10 CFR 50.73 reporting requirements. Licensee actions were documented in Condition Report CR-GGN-2002-1575. | ||
b. Findings No findings of significance were identified. | b. | ||
Findings No findings of significance were identified. | |||
.2 Loss of Residual Heat Removal Train A Shutdown Cooling a. | |||
Inspection Scope On September 16, 2002, the inspector observed GGNS operator performance when they responded to a RHR room sump Hi-Hi alarm and an unplanned transfer from RHR Train A shutdown cooling to Alternate Decay Heat Removal. The inspector reviewed the licensees response to the event to determine if operator response was in accordance with procedures and training. In addition, the inspector reviewed plant computer data and operator logs to further determine operator response. | |||
b. | |||
Findings No findings of significance were identified. | |||
1R15 Operability Evaluations (71111.15) | 1R15 Operability Evaluations (71111.15) | ||
a. Inspection Scope | a. | ||
Inspection Scope | |||
The inspectors selected four operability evaluations conducted by GGNS personnel during the report period involving risk-significant SSCs. The inspectors evaluated the technical adequacy of the operability determinations, determined whether appropriate compensatory measures were implemented, and determined whether GGNS personnel considered all other pre-existing conditions, as applicable. Additionally, the inspectors evaluated the adequacy of the GGNSs problem identification and resolution program as it applied to operability evaluations. Specific operability evaluations reviewed are listed below. | |||
* CR-GGN-2002-0755, Train A RHR system leakage | * CR-GGN-2002-0755, Train A RHR system leakage | ||
* | |||
CR-GGN-2002-1107, Postscram heatup and cooldown rate violations | |||
* | |||
CR-GGN-2002-1493, Standby service water system leakage | |||
* | |||
CR-GGN-2002-1628, Division III emergency diesel generator oil level b. | |||
Findings No findings of significance were identified. | |||
-8-1R16 Operator Workarounds (71111.16) | -8-1R16 Operator Workarounds (71111.16) | ||
.1 Review of Selected Operator Workarounds a. | |||
Inspection Scope The inspectors evaluated significant operator workarounds to determine if the functional capability of the system or human reliability in responding to an initiating event was affected. The inspectors evaluated the effect of operator workarounds on the operators ability to implement applicable abnormal and emergency operating procedures. The inspectors also reviewed the effect of the distraction caused by the operator workaround on operators ability to effectively control the plant. The following workaround was reviewed: | |||
* | |||
Significant Operator Workaround No. 3, dated 7/16/2002. Recirculation flow control valves are difficult to open during shifting of recirculation pumps to fast speed. | |||
b. | |||
Findings No findings of significance were identified. | |||
1R19 Postmaintenance Testing (71111.19) | 1R19 Postmaintenance Testing (71111.19) | ||
a. Inspection Scope The inspectors reviewed postmaintenance test procedures and associated testing activities for five selected risk-significant mitigating systems. In each case, the associated work orders and test procedures were reviewed against the attributes in Inspection Procedure 71111, Attachment 19, to determine the scope of the maintenance activity and determine if the testing was adequate to verify equipment operability. The reviewed activities were: | a. | ||
Inspection Scope The inspectors reviewed postmaintenance test procedures and associated testing activities for five selected risk-significant mitigating systems. In each case, the associated work orders and test procedures were reviewed against the attributes in Inspection Procedure 71111, Attachment 19, to determine the scope of the maintenance activity and determine if the testing was adequate to verify equipment operability. The reviewed activities were: | |||
MAI 299251, Control room air conditioning system, Train B | |||
MAI 299265, Standby gas treatment system, Train A | |||
MAI 313388, Reactor core isolation cooling (RCIC) system flow transmitter | |||
MAI 315222, Division I standby diesel generator restoration | |||
MAI 317583, Standby liquid control system, Train A b. | |||
Findings Isolation of main steam to the RCIC system occurred when GGNS maintenance personnel attempted to backfill the RCIC LDS's flow transmitter with a procedure that was inadequate for the job. The inspectors considered this inadequate maintenance procedure a Green NCV violation of Technical Specification 5.4.1.a. | |||
On May 31, 2002, GGNS operations personnel noticed that indications for the RCIC steam flow leakage detection Transmitter 1E31N083B was drifting towards the out of specification reading as indicated on its associated Trip Unit 1E31N683B. To correct | On May 31, 2002, GGNS operations personnel noticed that indications for the RCIC steam flow leakage detection Transmitter 1E31N083B was drifting towards the out of specification reading as indicated on its associated Trip Unit 1E31N683B. To correct | ||
-9-this, GGNS personnel issued MAI 313388 to backfill the transmitter and dispatched instrumentation and control (I&C) personnel to perform the work. These I&C technicians did not realize the process side of the transmitter was at reactor pressure and additionally, the work instructions did not include a step to note system pressures prior to commencing the detector backfill. As a result, the I&C technicians backfilled the transmitter without using a high pressure pump as required when backfilling a detector at reactor pressure. The technicians ended up purging the fluid from the transmitter lines with steam. When the transmitter was restored, fluid condensed in the sensing lines of the transmitter which the transmitter sensed as high steam flow. This made the transmitter effectively detect a steam leak in the RCIC steam line, and by design shut the RCIC steam line isolation Valve E31F063B, thereby rendering the RCIC system inoperable. | |||
The MAI utilized referenced Maintenance Procedure 07-S-13-48, "Filling, Venting, and Equalizing Sensing Lines," Revision 2, which gives generic guidance on how to backfill a differential pressure transmitter for generic backfilling guidance. This maintenance procedure did not provide a means to alert the I&C technicians as to what system pressures were prior to commencing maintenance. Since backfilling this detector normally occurs at off-rated conditions, the procedure was not tuned for the conditions at which it was performed. Such guidance would have provided the I&C technicians proper direction on how to satisfactorily proceed with backfilling this detector without isolating the RCIC system. | The MAI utilized referenced Maintenance Procedure 07-S-13-48, "Filling, Venting, and Equalizing Sensing Lines," Revision 2, which gives generic guidance on how to backfill a differential pressure transmitter for generic backfilling guidance. This maintenance procedure did not provide a means to alert the I&C technicians as to what system pressures were prior to commencing maintenance. Since backfilling this detector normally occurs at off-rated conditions, the procedure was not tuned for the conditions at which it was performed. Such guidance would have provided the I&C technicians proper direction on how to satisfactorily proceed with backfilling this detector without isolating the RCIC system. | ||
| Line 227: | Line 354: | ||
-10-1R20 Refueling and Other Outage Activities (71111.20) | -10-1R20 Refueling and Other Outage Activities (71111.20) | ||
a. Inspection Scope The inspectors observed refueling outage planning and execution activities. The inspectors review included scheduling, training, outage configuration management, decay heat removal operation and management, reactivity controls, inventory controls, tag out and clearance activities, foreign material exclusion management, and fuel movement and storage. Specific activities observed included: | a. | ||
Inspection Scope The inspectors observed refueling outage planning and execution activities. The inspectors review included scheduling, training, outage configuration management, decay heat removal operation and management, reactivity controls, inventory controls, tag out and clearance activities, foreign material exclusion management, and fuel movement and storage. Specific activities observed included: | |||
* | |||
Reactor scram and shutdown | |||
* | |||
Reactor cooldown and transition to shutdown cooling | |||
* | |||
Transition from Mode 3 (hot shutdown) to Mode 4 (cold shutdown) | |||
* | |||
Shutdown cooling and alternate decay heat removal operations | |||
* | |||
Operations with potential to drain the reactor vessel during control rod drive mechanism removal and replacement | |||
* | |||
Core alterations | |||
* | |||
Drywell inspection closeout activities | |||
* | |||
Jet Pump 13 removal and replacement | |||
* | |||
Valve B33 FO67B inspection and repair b. | |||
Findings No findings of significance were identified. | |||
1R22 Surveillance Testing (71111.22) | 1R22 Surveillance Testing (71111.22) | ||
a. | a. | ||
Inspection Scope The inspectors observed performance of surveillance test procedures and reviewed test data of five selected risk-significant SSCs to assess whether the SSCs satisfied the Technical Specifications, the Updated Final Safety Analysis Report, the Technical Requirements Manual, and licensee procedural requirements; and, to determine if the testing appropriately demonstrated that the SSCs were operationally ready and capable of performing their intended safety functions. The following tests were inspected: | |||
* | |||
06-CH-1B21-O-0002, "Reactor Coolant Routine Chemistry," Revision 104 | |||
Revision 104 b. Findings No findings of significance were identified. | * | ||
06-EL-1L11-Q-0001, "125 Volt Battery Bank All Cell Check," Revision 103 | |||
* | |||
06-OP-1P75-M-0001, "Standby Diesel Generator 11 Functional Test," | |||
-11-Revision 118 | |||
* | |||
06-OP-1R20-W-0001, Plant AC and DC Electrical Power Distribution Weekly Lineup, Revision 104 | |||
* | |||
06-OP-1T48-M-0001, "Standby Gas Treatment System A Operability," | |||
Revision 104 b. | |||
Findings No findings of significance were identified. | |||
1R23 Temporary Plant Modifications (71111.23) | 1R23 Temporary Plant Modifications (71111.23) | ||
a. Inspection Scope The inspectors reviewed the temporary alteration listed below to assess the following attributes: (1) the adequacy of the safety evaluation; (2) the consistency of the installation with the modification documentation; (3) the updating of drawings and procedures, as applicable; and, (4) the adequacy of the postinstallation testing. | a. | ||
Inspection Scope The inspectors reviewed the temporary alteration listed below to assess the following attributes: (1) the adequacy of the safety evaluation; (2) the consistency of the installation with the modification documentation; (3) the updating of drawings and procedures, as applicable; and, (4) the adequacy of the postinstallation testing. | |||
* No. 2002-006, Lifted lead for RCIC Valve E51F064 b. | |||
Findings No findings of significance were identified. | |||
Emergency Preparedness [EP] | Emergency Preparedness [EP] | ||
1EP6 Drill Observation (71114.06) | 1EP6 Drill Observation (71114.06) | ||
a. Inspection Scope On July 9, 2002, the inspectors observed a planned licensee emergency preparedness quarterly drill. The inspectors reviewed the drill scenario to determine if it reflected realistic plant configurations. The inspectors observed GGNS personnel at various locations during the exercise including the control room simulator, the technical support center, the emergency operations facility, and the operations support center. The inspectors primarily focused on the ability of the emergency response organization to properly classify the simulated emergency through recognition of emergency action levels, their ability to activate the station emergency plan and procedures, and their ability to make proper and timely notifications, as appropriate. | a. | ||
Inspection Scope On July 9, 2002, the inspectors observed a planned licensee emergency preparedness quarterly drill. The inspectors reviewed the drill scenario to determine if it reflected realistic plant configurations. The inspectors observed GGNS personnel at various locations during the exercise including the control room simulator, the technical support center, the emergency operations facility, and the operations support center. The inspectors primarily focused on the ability of the emergency response organization to properly classify the simulated emergency through recognition of emergency action levels, their ability to activate the station emergency plan and procedures, and their ability to make proper and timely notifications, as appropriate. | |||
b. | |||
Findings No findings of significance were identified. | |||
-12-3. | |||
SAFEGUARDS Cornerstone: Physical Protection [PP] | |||
3PP3 Response to Contingency Events (71130.03) | 3PP3 Response to Contingency Events (71130.03) | ||
The Office of Homeland Security (OHS) developed a Homeland Security Advisory System (HSAS) to disseminate information regarding the risk of terrorist attacks. The HSAS implemented five color-coded threat conditions with a description of corresponding actions at each level. NRC Regulatory Information Summary (RIS) 2002-12a, dated August 19, 2002, NRC Threat Advisory and Protective Measures System, discusses the HSAS and provides additional information on protective measures to licensees. | The Office of Homeland Security (OHS) developed a Homeland Security Advisory System (HSAS) to disseminate information regarding the risk of terrorist attacks. The HSAS implemented five color-coded threat conditions with a description of corresponding actions at each level. NRC Regulatory Information Summary (RIS) 2002-12a, dated August 19, 2002, NRC Threat Advisory and Protective Measures System, discusses the HSAS and provides additional information on protective measures to licensees. | ||
a. Inspection Scope On September 10, 2002, the NRC issued a Safeguards Advisory to reactor licensees to implement the protective measures described in RIS 2002-12a in response to the Federal government declaration of threat level orange. Subsequently, on September 24, 2002, the OHS downgraded the national security threat condition to yellow and a corresponding reduction in the risk of a terrorist threat. | a. | ||
Inspection Scope On September 10, 2002, the NRC issued a Safeguards Advisory to reactor licensees to implement the protective measures described in RIS 2002-12a in response to the Federal government declaration of threat level orange. Subsequently, on September 24, 2002, the OHS downgraded the national security threat condition to yellow and a corresponding reduction in the risk of a terrorist threat. | |||
The inspectors interviewed licensee personnel and security staff, observed the conduct of security operations, and assessed licensee implementation of the threat level orange protective measures. Inspection results were communicated to the region and headquarters security staff for further evaluation. | The inspectors interviewed licensee personnel and security staff, observed the conduct of security operations, and assessed licensee implementation of the threat level orange protective measures. Inspection results were communicated to the region and headquarters security staff for further evaluation. | ||
b. Findings No findings of significance were identified. | b. | ||
Findings No findings of significance were identified. | |||
4. OTHER ACTIVITIES [OA] | 4. | ||
OTHER ACTIVITIES [OA] | |||
4OA1 Performance Indicator Verification (71151) | 4OA1 Performance Indicator Verification (71151) | ||
a. Inspection Scope The inspectors verified the accuracy and completeness of the data used to calculate and report performance indicator information for three indicators from the third calendar quarter 2001 through the second calendar quarter 2002. The inspectors used Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," | a. | ||
Inspection Scope The inspectors verified the accuracy and completeness of the data used to calculate and report performance indicator information for three indicators from the third calendar quarter 2001 through the second calendar quarter 2002. The inspectors used Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," | |||
Revision 2, as guidance and interviewed licensee personnel responsible for compiling the information. | Revision 2, as guidance and interviewed licensee personnel responsible for compiling the information. | ||
* Heat removal system (RCIC system) unavailability | |||
* | |||
High pressure injection system (high pressure core spray system) unavailability | |||
* | |||
Safety system functional failures The inspectors also performed routine checks, while on tours throughout the plant, to | |||
-13-ensure that locked high radiation areas were properly secured. | |||
b. | |||
Findings No findings of significance were identified. | |||
4OA2 Identification and Resolution of Problems (71152) | 4OA2 Identification and Resolution of Problems (71152) | ||
a | a. | ||
b. Findings No other findings of significance were identified. | Inspection Scope The inspectors conducted in-depth reviews of the problem identification and resolution aspects of two issues. The inspectors reviewed the GGNS personnels evaluations of operability and reportability for the issues, verified corrective actions were appropriately focused to correct the problems, and that those corrective actions were completed in a manner commensurate with the safety significance of the issue. The scope of the reviews also included determination whether identification was made in a timely manner, whether proper extent of condition was reviewed, and whether the corrective actions were completed in a manner commensurate with safety. The following two issues were reviewed: | ||
* | |||
Primary containment isolation Valve E12F044A being discovered partially opened on two occasions | |||
* | |||
Control room air conditioning unit Train B repetitive failures in June and July 2002 The inspectors also reviewed an issue which involved problem identification and resolution causes and documented it as a licensee-identified violation in Section 40A7 of this report. | |||
b. | |||
Findings No other findings of significance were identified. | |||
4OA3 Event Followup (71153) | 4OA3 Event Followup (71153) | ||
.1 (Closed) Licensee Event Report 50-416/02-002-00, "RHR System Pressure Higher Than Normal Rendering Primary Containment Isolation Valve (PCIV) Inoperable For About 11 Days" On April 7, 2002, the licensee noted from control room indications that the fill valve for the RHR system from the condensate and refueling water transfer system was not completely shut. Further inspection by the licensee revealed that this valve was also a primary containment isolation valve and had been left in this state for about 11 days. | |||
Based on the indeterminate amount of leakage from the valve in its as-found state, GGNS personnel declared the primary containment isolation valve inoperable. The time period for the declared inoperability was in excess of the allowed outage time set forth in Technical Specification 3.6.1.3, therefore the licensee wrote this licensee event report and the finding was captured in the licensee's corrective action program in Condition | Based on the indeterminate amount of leakage from the valve in its as-found state, GGNS personnel declared the primary containment isolation valve inoperable. The time period for the declared inoperability was in excess of the allowed outage time set forth in Technical Specification 3.6.1.3, therefore the licensee wrote this licensee event report and the finding was captured in the licensee's corrective action program in Condition | ||
-14-Report CR-GGN-2002-0755. | |||
The inspectors reviewed the licensees safety assessment, condition report corrective actions, and troubleshooting efforts associated with this licensee event report and considered this issue a minor violation of Technical Specification 3.6.1.3. | The inspectors reviewed the licensees safety assessment, condition report corrective actions, and troubleshooting efforts associated with this licensee event report and considered this issue a minor violation of Technical Specification 3.6.1.3. | ||
| Line 311: | Line 486: | ||
4OA7 Licensee-Identified Violations The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV. | 4OA7 Licensee-Identified Violations The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV. | ||
-15-10 CFR 50, Appendix B, Criterion XVI states in part that measures shall be established to assure that conditions adverse to quality, such as malfunctions, are promptly identified and corrected. On May 31, 2002, during a monthly surveillance run, the standby gas treatment system Train A enclosure building fan failed to start due to ineffective actions to correct the failure of the fan to start following a previous system outage on May 30, 2002. This condition is described in the licensees corrective action program in Condition Reports CR-GGN-2002-0942 and CR-GGN-2002-0948. Because only the radiological barrier function of the system was degraded, this violation is not more than of very low safety significance, and is being treated as a NCV. | -15- | ||
10 CFR 50, Appendix B, Criterion XVI states in part that measures shall be established to assure that conditions adverse to quality, such as malfunctions, are promptly identified and corrected. On May 31, 2002, during a monthly surveillance run, the standby gas treatment system Train A enclosure building fan failed to start due to ineffective actions to correct the failure of the fan to start following a previous system outage on May 30, 2002. This condition is described in the licensees corrective action program in Condition Reports CR-GGN-2002-0942 and CR-GGN-2002-0948. Because only the radiological barrier function of the system was degraded, this violation is not more than of very low safety significance, and is being treated as a NCV. | |||
ATTACHMENT PARTIAL LIST OF PERSONS CONTACTED C. Abbott, Quality Assurance Supervisor D. Barfield, Manager, System Engineering R. Barnes, Manager, Training and Development C. Bottemiller, Manager, Plant Licensing K. Christian, Superintendent, Mechanical Maintenance M. Cross, ISI Coordinator, Quality Assurance and Nondestructive Examination W. Deck, Security Superintendent W. Eaton, Vice President, Operations J. Edwards, General Manager, Plant Operations C. Ellsaesser, Manager, Corrective Action and Assessment A. Goel, Senior Engineer, Plant Licensing M. Guynn, Manager, Emergency Preparedness R. Moomaw, Manager, Outage Planning and Scheduling M. Mottsen, Supervisor, Engineering J. Roberts, Director, Nuclear Safety Assurance J. Robertson, Manager, Quality Assurance E. Rogers, Manager, Site Support M. Rohrer, Manager, Maintenance G. Sparks, Manager, Operations D. Watt, Site Welding Engineer, Engineering Programs and Components D. Wiles, Director, Engineering R. Wilson, Superintendent, Radiation Protection H. Yeldell, Manager, Design Engineering ITEMS OPENED, CLOSED, AND DISCUSSED Opened 05000416/2002-004-01 NCV Performance of maintenance using an inadequate procedure leads to isolation of the reactor core cooling isolation system (Section 1R19) | ATTACHMENT PARTIAL LIST OF PERSONS CONTACTED C. Abbott, Quality Assurance Supervisor D. Barfield, Manager, System Engineering R. Barnes, Manager, Training and Development C. Bottemiller, Manager, Plant Licensing K. Christian, Superintendent, Mechanical Maintenance M. Cross, ISI Coordinator, Quality Assurance and Nondestructive Examination W. Deck, Security Superintendent W. Eaton, Vice President, Operations J. Edwards, General Manager, Plant Operations C. Ellsaesser, Manager, Corrective Action and Assessment A. Goel, Senior Engineer, Plant Licensing M. Guynn, Manager, Emergency Preparedness R. Moomaw, Manager, Outage Planning and Scheduling M. Mottsen, Supervisor, Engineering J. Roberts, Director, Nuclear Safety Assurance J. Robertson, Manager, Quality Assurance E. Rogers, Manager, Site Support M. Rohrer, Manager, Maintenance G. Sparks, Manager, Operations D. Watt, Site Welding Engineer, Engineering Programs and Components D. Wiles, Director, Engineering R. Wilson, Superintendent, Radiation Protection H. Yeldell, Manager, Design Engineering ITEMS OPENED, CLOSED, AND DISCUSSED Opened 05000416/2002-004-01 NCV Performance of maintenance using an inadequate procedure leads to isolation of the reactor core cooling isolation system (Section 1R19) | ||
Closed 05000416/2002-002-00 LER RHR system pressure higher than normal rendering primary containment isolation valve (PCIV) inoperable for about 11 days (Section 4OA3) | Closed 05000416/2002-002-00 LER RHR system pressure higher than normal rendering primary containment isolation valve (PCIV) inoperable for about 11 days (Section 4OA3) | ||
05000416/2002-003-00 LER Reactor scram due to loss of service Transformer 21 (Section 4OA3) | 05000416/2002-003-00 LER Reactor scram due to loss of service Transformer 21 (Section 4OA3) | ||
05000416/2002-004-01 NCV Performance of maintenance using an inadequate procedure leads to isolation of the reactor core cooling isolation (Section 1R19) | 05000416/2002-004-01 NCV Performance of maintenance using an inadequate procedure leads to isolation of the reactor core cooling isolation (Section 1R19) | ||
-2-LIST OF DOCUMENTS REVIEWED Procedures: | |||
Emergency Plan Procedure 10-S-01-1, "Activation of the Emergency Plan," Revision 109 Emergency Plan Procedure 10-S-01-6, "Notification of Offsite Agencies and Plant On-call Emergency Personnel," Revision 36 Emergency Plan Procedure 10-S-01-33, "Emergency Operations Facility Operations," | Emergency Plan Procedure 10-S-01-1, "Activation of the Emergency Plan," Revision 109 Emergency Plan Procedure 10-S-01-6, "Notification of Offsite Agencies and Plant On-call Emergency Personnel," Revision 36 Emergency Plan Procedure 10-S-01-33, "Emergency Operations Facility Operations," | ||
Revision 11 General Maintenance Instruction 07-S-12-44, "Station Battery Pilot Cell Inspection," Revision 11 Grand Gulf Nuclear Station Unit 1 Fire Preplans, Volumes 1 and 2, Revision 11 Off-Normal Event Procedure 05-S-01-EP2, "EP-2A, RPV Control - ATWS," Revision dated April 24, 2001 Off-Normal Event Procedure 05-1-02-VI-1, "Flooding," Revision 102 System Operating Instruction 04-1-01-L11-1, "Plant DC Systems," Revision 115 QAI 9.30, Liquid Penetrant Examination, Revision 5 QAI 9.15, Magnetic Particle Examination, Revision 7 NDE 9.24, Manual Ultrasonic Examination of Reactor Vessel Ligament Areas, Revision 2 NDE 9.26, Ultrasonic Manual Examination of Class 1 Reactor Vessel Welds, Revision 2 NDE 9.23, Ultrasonic Examination of Austenitic Piping Welds, Revision 2 NDE 9.07, Straight Beam Ultrasonic Examination of Bolts and Studs, Revision 2 NDE 9.25, Manual Ultrasonic Examination of Nozzle Radii, Revision 2 NDE 9.04, Ultrasonic Examination of Ferritic Piping Welds, Revision 2 NDE 9.55, Radiographic Examination of ASME, ANSI, AWS, API, AWWA Welds and Components, Revision 0 Condition Reports: | Revision 11 General Maintenance Instruction 07-S-12-44, "Station Battery Pilot Cell Inspection," Revision 11 Grand Gulf Nuclear Station Unit 1 Fire Preplans, Volumes 1 and 2, Revision 11 Off-Normal Event Procedure 05-S-01-EP2, "EP-2A, RPV Control - ATWS," Revision dated April 24, 2001 Off-Normal Event Procedure 05-1-02-VI-1, "Flooding," Revision 102 System Operating Instruction 04-1-01-L11-1, "Plant DC Systems," Revision 115 QAI 9.30, Liquid Penetrant Examination, Revision 5 QAI 9.15, Magnetic Particle Examination, Revision 7 NDE 9.24, Manual Ultrasonic Examination of Reactor Vessel Ligament Areas, Revision 2 NDE 9.26, Ultrasonic Manual Examination of Class 1 Reactor Vessel Welds, Revision 2 NDE 9.23, Ultrasonic Examination of Austenitic Piping Welds, Revision 2 NDE 9.07, Straight Beam Ultrasonic Examination of Bolts and Studs, Revision 2 NDE 9.25, Manual Ultrasonic Examination of Nozzle Radii, Revision 2 NDE 9.04, Ultrasonic Examination of Ferritic Piping Welds, Revision 2 NDE 9.55, Radiographic Examination of ASME, ANSI, AWS, API, AWWA Welds and Components, Revision 0 Condition Reports: | ||
1999-1976 | 1999-1976 2002-0494 2002-0755 2002-0823 2002-0912 2002-0933 2002-1106 2002-1115 2002-1149 2002-1240 2002-1423 2002-1454 | ||
-3-Maintenance Action Items: | |||
250736 | 250736 304244 307083 308112 308461 310606 312342 313508 314272 315281 317065 317683 318000 318422 318801 319002 319075 Examinations Reviewed: | ||
System | System Component/Weld Identification Examination Method Reactor Coolant System B13-0910-89 Ultrasonic Examination Reactor Coolant System B13-0904-89 Ultrasonic Examination Reactor Coolant System B13-0909-89 Ultrasonic Examination Feedwater System B21-0746-92 Ultrasonic Examination Feedwater System B21-0433-89 Ultrasonic Examination Feedwater System B21-0442-89 Ultrasonic Examination Feedwater System B21-0452-89 Ultrasonic Examination Feedwater System B21-1078-90 Dye Penetrant Feedwater System B21-0469-89 Ultrasonic Examination Feedwater System B21-0440-89 Magnetic Particle Feedwater System B21-0441-89 Dye Penetrant Feedwater System B21-0349-95 Magnetic Particle Reactor Recirculation B33-1236-92 Ultrasonic Examination Reactor Recirculation B33-1124-92 Ultrasonic Examination Reactor Recirculation B33-0192-89 Dye Penetrant Reactor Recirculation B33-0971-89 Ultrasonic Examination Reactor Recirculation B33-0202-89 Dye Penetrant Control Rod Drive C11-0528-90 Ultrasonic Examination Control Rod Drive C11-0550-90 Ultrasonic Examination | ||
-4-Other Miscellaneous Documents: | |||
Calculation EC-Q1L11-91011, "Station Blackout Evaluation of 125 VDC Division I Battery," | Calculation EC-Q1L11-91011, "Station Blackout Evaluation of 125 VDC Division I Battery," | ||
Revision 0 Calculation EC-Q1L21-90047, "Sizing of 125 VDC Division II Battery and Chargers," Revision 2 | Revision 0 Calculation EC-Q1L21-90047, "Sizing of 125 VDC Division II Battery and Chargers," Revision 2 | ||
"Detroit Diesel Engines Series 149 Service Manual," Revision 4/77 Kohler Generators 500R0ZD Operating Instructions | "Detroit Diesel Engines Series 149 Service Manual," Revision 4/77 Kohler Generators 500R0ZD Operating Instructions | ||
}} | }} | ||
Latest revision as of 15:22, 16 January 2025
| ML022980071 | |
| Person / Time | |
|---|---|
| Site: | Grand Gulf |
| Issue date: | 10/24/2002 |
| From: | Johnson W NRC/RGN-IV/DRP/RPB-A |
| To: | Eaton W Entergy Operations |
| References | |
| -nr IR-02-004 | |
| Download: ML022980071 (25) | |
Text
October 24, 2002
SUBJECT:
GRAND GULF NUCLEAR STATION NRC INTEGRATED INSPECTION REPORT 50-416/02-04
Dear Mr. Eaton:
On September 28, 2002, the NRC completed an inspection at your Grand Gulf Nuclear Station, facility. The enclosed integrated report documents the inspection findings which were discussed on October 4, 2002, with you and other members of your staff.
This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
Within these areas, the inspection consisted of selected examination of procedures and representative records, observations of activities, and interviews with personnel.
Based on the results of this inspection, the NRC has identified an issue that was evaluated under the risk significance determination process as having very low safety significance (Green).
The NRC has also determined that a violation is associated with this issue. This violation is being treated as a noncited violation (NCV), consistent with Section VI.A of the Enforcement Policy. The NCV is described in the subject inspection report. If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Grand Gulf Nuclear Station facility.
In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Entergy Operations, Inc.
-2-Should you have any questions concerning this inspection, we will be pleased to discuss them with you.
Sincerely,
/RA/
William D. Johnson, Chief Project Branch A Division of Reactor Projects Docket: 50-416 License: NPF-29 Enclosure NRC Inspection Report 50-416/02-04 cc w/enclosure:
Executive Vice President and Chief Operating Officer Entergy Operations, Inc.
P.O. Box 31995 Jackson, Mississippi 39286-1995 Wise, Carter, Child & Caraway P.O. Box 651 Jackson, Mississippi 39205 Winston & Strawn 1400 L Street, N.W. - 12th Floor Washington, DC 20005-3502 Director Division of Solid Waste Management Mississippi Department of Natural Resources P.O. Box 10385 Jackson, Mississippi 39209 President, District 1 Claiborne County Board of Supervisors P.O. Box 339 Port Gibson, Mississippi 39150
Entergy Operations, Inc.
-3-General Manager Grand Gulf Nuclear Station Entergy Operations, Inc.
P.O. Box 756 Port Gibson, Mississippi 39150 The Honorable Richard Ieyoub Attorney General Department of Justice State of Louisiana P.O. Box 94005 Baton Rouge, Louisiana 70804-9005 Office of the Governor State of Mississippi Jackson, Mississippi 39201 Mike Moore, Attorney General Frank Spencer, Asst. Attorney General State of Mississippi P.O. Box 22947 Jackson, Mississippi 39225 Dr. F. E. Thompson, Jr.
State Health Officer State Board of Health P.O. Box 1700 Jackson, Mississippi 39215 Robert W. Goff, Program Director Division of Radiological Health Mississippi Dept. of Health P.O. Box 1700 Jackson, Mississippi 39215-1700 Vice President Operations Support Entergy Operations, Inc.
P.O. Box 31995 Jackson, Mississippi 39286-1995 Director, Nuclear Safety and Regulatory Affairs Entergy Operations, Inc.
P.O. Box 756 Port Gibson, Mississippi 39150
Entergy Operations, Inc.
-4-Electronic distribution by RIV:
Regional Administrator (EWM)
DRP Director (KEB)
DRS Director (EEC)
Senior Resident Inspector (TLH4)
Branch Chief, DRP/A (WDJ)
Senior Project Engineer, DRP/A (CJP)
Staff Chief, DRP/TSS (PHH)
RITS Coordinator (NBH)
Scott Morris (SAM1)
GG Site Secretary (MJS)
Dale Thatcher (DFT)
R;\\_GG\\2002\\GG2002-04RP-TLH.wpd RIV:RI:DRP/A SRI:DRP/A DRS/PSB DRS/EMB PE:DRP/A RWDeese TLHoeg DRCarter CSMarschall JMKeeton E-WDJohnson E-WDJohnson E-WDJohnson
/RA/
/RA/
10/22/02 10/22/02 10/22/02 10/23/02 10/22/02 SPE:DRP/A C:DRP/A CJPaulk WDJohnson
/RA/
/RA/
10/22/02 10/24/02 OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax
ENCLOSURE U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket:
50-416 License:
NPF-29 Report No:
50-416/02-04 Licensee:
Entergy Operations, Inc.
Facility:
Grand Gulf Nuclear Station Location:
Waterloo Road Port Gibson, Mississippi 39150 Dates:
June 30 through September 28, 2002 Inspectors:
T. L. Hoeg, Senior Resident Inspector D. R. Carter, Health Physicist R. W. Deese, Resident Inspector J. M. Keeton, Project Engineer C. J. Paulk, Senior Project Engineer W. C. Sifre, Reactor Inspector Approved By:
W. D. Johnson, Chief, Project Branch A Division of Reactor Projects Attachment:
Supplemental Information
SUMMARY OF FINDINGS IR 05000416-02-04, Entergy Operations, Inc., on 6/30/02 - 09/28/02; Grand Gulf Nuclear Station. Postmaintenance testing, surveillance testing.
The inspection was conducted by resident inspectors and a regional reactor inspector. The inspectors identified one Green noncited violation. The significance of any findings are indicated by their color (Green, White, Yellow, or Red) using IMC 0609 "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649,
"Reactor Oversight Process," Revision 3, dated July 2000.
A.
Inspector Identified Findings Cornerstone: Mitigating Systems
Green. The licensee failed to establish appropriate instructions for the circumstances when backfilling the reactor core isolation cooling high steam flow transmitter. This resulted in technicians improperly backfilling the detector. This caused the detector to isolate steam to the reactor core isolation cooling turbine, rendering the system inoperable.
This violation of Technical Specification 5.4.1 is noncited in accordance with Section VI.A of the NRC's Enforcement Policy, and is in the licensee's corrective action program (CR-GGN-2002-0947). The finding was of very low safety significance because although the reactor core isolation cooling system was inoperable, all other remaining mitigating systems remained operable and the duration of the system inoperability was short (Section 1R19).
B.
Licensee Identified Findings A violation of very low safety significance, which was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and its corrective action tracking number are listed in Section 4OA7 of this report.
Report Details Summary of Plant Status: The plant began the inspection period at 100 percent rated thermal power and subsequently performed a planned power reduction to 80 percent on June 30, 2002, for initial startup of the auxiliary cooling tower. The plant was then operated at or near 100 percent rated thermal power except for periodic planned power reductions for monthly control rod exercising and periodic control rod pattern adjustments until July 25, when a partial loss of radial well pumping capability necessitated a power reduction to 78 percent of rated power. Following the recovery of all radial wells, the plant returned to 100 percent power and remained there until August 5, when the plant began coasting down in power. The coastdown ended on September 13, with the plant at 84 percent rated thermal power when the plant entered a refueling outage. The plant remained shutdown in this outage for the remainder of the inspection period.
1.
REACTOR SAFETY Initiating Events, Mitigating Systems, Barrier Integrity [Reactor - R]
1R01 Adverse Weather Protection (71111.01)
a.
Inspection Scope The inspectors reviewed one sample of Grand Gulf Nuclear Station (GGNS) personnels protection of the three divisions of the 125 Volt dc engineered safety features (ESF)
batteries for sustained hot weather conditions since these components are housed in rooms that are ventilated but not air conditioned. This review included walkdowns of the battery rooms focusing on hot weather susceptibilities, reviews of the systems designed ventilation features, and a review of the licensees actions to ensure the batteries remain operable in hot weather. Technical Manual "C&D Station Battery Installation and Operating Instructions," dated October 12, 1995, was also reviewed to check the vendors recommendations for sustained battery operations at higher than the 77 F reference temperature.
b.
Findings No findings of significance were identified.
1R04 Equipment Alignment
.1 Partial System Walkdowns (71111.04)
a.
Inspection Scope The inspectors performed partial system walkdown inspections and reviews of a train in each of three systems important to reactor safety in order to verify the operability of the systems. The inspectors reviewed system operating instructions, system valve and breaker lineups, operator logs, and control room indications. The inspectors also verified valves, breakers, and control circuits were in their required positions for operability. The following systems were inspected:
-2-
Emergency diesel generator, Division I
Low pressure core spray system
Standby service water system, Train A b.
Findings No findings of significance were identified.
.2 Semi-Annual Complete System Walkdown (71111.04S)
a.
Inspection Scope During the week of July 22, 2002, the inspectors performed a complete walkdown of the Division II emergency diesel generator to determine if there were any discrepancies between the actual equipment alignment versus what was procedurally required. During the walkdown, System Operating Instruction 04-1-01-P75-1, "Standby Diesel Generator System," Revision 62, Surveillance Procedure 06-OP-1P75-V-0013, "Standby Diesel Generator (SDG) 12 Operability Verification," Revision 103, and Drawing M-1070B,
"Standby Diesel Generator System," Revision 30, were used by the inspectors to verify major diesel generator components were correctly labeled and aligned. The inspectors also reviewed open condition reports on the system for any deficiencies that could affect the ability of the system to perform its design function. Documentation associated with control room deficiencies, temporary modifications, operator workarounds, and items tracked by plant engineering were also reviewed to assess their collective impact on system operation.
b.
Findings No findings of significance were identified.
1R05 Fire Protection (71111.05)
.1 Quarterly Tours (71111.05Q)
a.
Inspection Scope The inspectors reviewed area fire plans and performed walkdowns of six plant areas to assess the materiel condition and operational status of fire detection, suppression systems and equipment; the materiel condition of fire barriers; and the control of transient combustibles. Specific risk-significant plant areas included:
Division III emergency diesel generator room, Room 1D304
Division III switchgear room, Room 0C210
Electrical penetration room, Room 1A318
ESF Heating, ventilation, and air conditioning equipment room, Room 0C302
Residual heat removal (RHR) Pump C Room 1A118
Standby service water Pump B Room 2M110
-3-b.
Findings No findings of significance were identified.
.2 Annual Drill Observation (71111.05A)
a.
Inspection Scope On August 29, 2002, the inspectors observed a fire brigade drill staged in Room 0C403, computer and control panel room, to evaluate the readiness of the fire brigade to fight fires. The inspectors reviewed the strategies and information in Fire Preplan C-10,
"Computer and Control Panels, Room 0C403, Area 25A," Revision 11, to verify if it was consistent with the fire protection design features, fire area boundaries, and combustible loading assumptions shown in the fire protection plan. The inspectors observed the fire brigade members: (1) donning protective clothing, (2) selecting turnout gear, (3) entering the fire zone, (4) using the fire preplan strategies, and (5) communicating with the control room staff. The inspectors observed the fire fighting equipment brought to the fire scene to evaluate whether sufficient equipment was available for the simulated fire. The inspectors observed fire fighting directions and radio communications between the brigade leader, brigade members, and the control room.
b.
Findings No findings of significance were identified.
1R06 Flood Protection (71111.06)
.1 Internal Flooding a.
Inspection Scope The inspectors reviewed one sample of the GGNSs internal flooding protection features associated with the general flood protection measures for RHR Pump C room. The inspectors also reviewed specific flood protection measures associated with Maintenance Action Item (MAI) 307083 for the cleaning of the auxiliary decay heat removal heat exchangers which are housed in the RHR Pump C room. In order to clean the heat exchangers, the flood door for the RHR Pump C room was propped open to facilitate the necessary equipment. The inspectors performed a walkdown of the area reviewing internal flooding vulnerabilities, questioned maintenance personnel on contingencies for having the door propped open, and reviewed the protective features and procedures for mitigating the impact of any flooding.
b.
Findings No findings of significance were identified.
-4-
.2 External Flooding a.
Inspection Scope The inspectors reviewed the Technical Requirements Manual Specification 6.7.5 and performed visual inspections of Culvert Number 1, examining its blockage and slope.
The inspectors also reviewed flood protection measures for external sources as described in the Updated Final Safety Analysis Report and Calculation C-A-254.5
"Evaluation of the Effect of Predictive Maximum Precipitation Flood Levels Above Elevation 133 Feet on Safe Plant Operation, Revision 1, and the associated Supplement 1, Revision 0, to that calculation, and then performed walkdowns to verify that the assumptions made in the external flooding analyses remained valid.
b.
Findings No findings of significance were identified.
1R08 Inservice Inspection Activities (71111.08)
.1 Performance of Nondestructive Examination (NDE) Activities a.
Inspection Scope The inspector requested and reviewed the NDE records for work that was performed for the current outage at the Grand Gulf Nuclear Station. The inspector also observed the following ultrasonic and magnetic particle examinations:
C11-G1010-W30 Control Rod Drive System
E51-G004-W29 Reactor Core Isolation Coolant System The inspector reviewed two weld repairs and two indications that were accepted for continued service. They were performed in accordance with ASME Code requirements.
The inspector reviewed licensee NDE and contractor personnel qualification and certification records to determine if the NDE personnel were certified to perform the above examinations. The inspector also reviewed ultrasonic calibration records to verify acceptability to ASME Code requirements.
The inspector reviewed the implementation of the containment inservice inspection program plan against the requirements of ASME Section XI, Subsection IWE.
b.
Findings No findings of significance were identified.
-5-
.2 Problem Identification and Resolution a.
Inspection Scope The inspector performed a detailed review of a sample of condition reports initiated within the past 2 years in the area of inservice inspection activities. The review was conducted to ascertain that the plant personnel were identifying performance issues within the inservice inspection program. This review assessed the effectiveness of cause determination, corrective action, and the adequacy of the plant personnels effort to identify transportability and generic issues. The review also assessed the effectiveness of the plant personnels effort to identify and address programmatic issues within the inservice inspection program.
b.
Findings No findings of significance were identified.
1R11 Licensed Operator Requalification (71111.11Q)
a.
Inspection Scope On August 1, 2002, the inspectors observed one session of licensed operator requalification training activities in the simulator to assess the licensee's effectiveness in conducting the requalification program and to verify that licensed individuals received the appropriate level of training required to maintain their licenses. The observed training consisted of establishing shutdown cooling and other nonroutine activities in preparation for the refueling outage. The inspectors also observed the post-training critique conducted by the training instructor and the shift manager to verify that weak areas observed during simulator operations were appropriately identified for additional training.
b.
Findings No findings of significance were identified.
1R12 Maintenance Rule Implementation (71111.12Q)
a.
Inspection Scope The inspectors reviewed performance-based problems involving three selected in-scope structures, systems, or components (SSCs) to assess the effectiveness of the Maintenance Rule Program. Reviews focused on: (1) proper Maintenance Rule scoping in accordance with 10 CFR 50.65; (2) characterization of failed SSCs; (3) safety significance classifications; (4) 10 CFR 50.65 (a)(1) and (a)(2) classifications; and, (5) the appropriateness of performance criteria for SSCs classified as (a)(2), and goals and corrective actions for SSCs classified as (a)(1). The inspectors reviewed the most recent system health reports and system functional failures for the last two years. The following conditions were reviewed:
-6-
Containment Isolation Valve E12F044A inoperability
Control rod drive system failures for Control Rods 12-13 and 60-37
Control room air conditioning Train B operational failures b.
Findings No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)
a.
Inspection Scope Throughout the inspection period, the inspectors reviewed weekly and daily work schedules to determine when risk-significant activities were scheduled. The inspectors discussed five selected activities with operations and work control personnel regarding risk evaluations and overall plant configuration control. The inspectors discussed emergent work issues with work control center personnel and reviewed the prioritization of scheduled activities. The inspectors verified the performance of plant risk assessments related to planned and emergent maintenance activities as required by 10 CFR 50.65(a)(4) and Plant Procedure 01-S-18-6, "Risk Assessment of Maintenance Activities," Revision 1.
Specific maintenance items reviewed during this period included:
MAI 297570, Hydrogen Recombiner B
MAI 307035, Low pressure core spray system
MAI 315778, Train B suppression pool makeup system
MAI 316476, Train A RHR system
MAI 318122, Instrument air system b.
Findings No findings of significance were identified.
1R14 Personnel Performance During Nonroutine Events (71111.14)
.1 Loss of Spent Fuel Pool Cooling a.
Inspection Scope On August 22, 2002, the plant experienced a loss of spent fuel pool cooling. The leak detection system (LDS) isolated and secured the fuel pool cooling and clean-up system when the LDS standpipe did not drain quickly enough after water was drained into the standpipe following restoration of a maintenance lineup. GGNS personnel investigated and discovered that the standpipe drain line was blocked and not allowing the standpipe to drain. The standpipe sensed this high level for an extended time and LDS logic interpreted this as a leak that the drain line could not keep up with and by design secured the running spent fuel pool cooling pump. GGNS personnel were able to assess the cause of the pump securing and restore fuel pool cooling in 44 minutes
-7-without any noticeable rise in fuel pool temperature. The inspectors responded to the plant and observed the recovery lineup of the fuel pool cooling system. The inspector reviewed Off-Normal Event Procedure 05-1-02-III-1, "Inadequate Decay Heat Removal,"
Revision 24, along with GGNS personnels actions for procedural compliance. The inspectors also reviewed licensee actions with regard to 10 CFR 50.72 and 10 CFR 50.73 reporting requirements. Licensee actions were documented in Condition Report CR-GGN-2002-1575.
b.
Findings No findings of significance were identified.
.2 Loss of Residual Heat Removal Train A Shutdown Cooling a.
Inspection Scope On September 16, 2002, the inspector observed GGNS operator performance when they responded to a RHR room sump Hi-Hi alarm and an unplanned transfer from RHR Train A shutdown cooling to Alternate Decay Heat Removal. The inspector reviewed the licensees response to the event to determine if operator response was in accordance with procedures and training. In addition, the inspector reviewed plant computer data and operator logs to further determine operator response.
b.
Findings No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a.
Inspection Scope
The inspectors selected four operability evaluations conducted by GGNS personnel during the report period involving risk-significant SSCs. The inspectors evaluated the technical adequacy of the operability determinations, determined whether appropriate compensatory measures were implemented, and determined whether GGNS personnel considered all other pre-existing conditions, as applicable. Additionally, the inspectors evaluated the adequacy of the GGNSs problem identification and resolution program as it applied to operability evaluations. Specific operability evaluations reviewed are listed below.
- CR-GGN-2002-0755, Train A RHR system leakage
CR-GGN-2002-1107, Postscram heatup and cooldown rate violations
CR-GGN-2002-1493, Standby service water system leakage
CR-GGN-2002-1628, Division III emergency diesel generator oil level b.
Findings No findings of significance were identified.
-8-1R16 Operator Workarounds (71111.16)
.1 Review of Selected Operator Workarounds a.
Inspection Scope The inspectors evaluated significant operator workarounds to determine if the functional capability of the system or human reliability in responding to an initiating event was affected. The inspectors evaluated the effect of operator workarounds on the operators ability to implement applicable abnormal and emergency operating procedures. The inspectors also reviewed the effect of the distraction caused by the operator workaround on operators ability to effectively control the plant. The following workaround was reviewed:
Significant Operator Workaround No. 3, dated 7/16/2002. Recirculation flow control valves are difficult to open during shifting of recirculation pumps to fast speed.
b.
Findings No findings of significance were identified.
1R19 Postmaintenance Testing (71111.19)
a.
Inspection Scope The inspectors reviewed postmaintenance test procedures and associated testing activities for five selected risk-significant mitigating systems. In each case, the associated work orders and test procedures were reviewed against the attributes in Inspection Procedure 71111, Attachment 19, to determine the scope of the maintenance activity and determine if the testing was adequate to verify equipment operability. The reviewed activities were:
MAI 299251, Control room air conditioning system, Train B
MAI 299265, Standby gas treatment system, Train A
MAI 313388, Reactor core isolation cooling (RCIC) system flow transmitter
MAI 315222, Division I standby diesel generator restoration
MAI 317583, Standby liquid control system, Train A b.
Findings Isolation of main steam to the RCIC system occurred when GGNS maintenance personnel attempted to backfill the RCIC LDS's flow transmitter with a procedure that was inadequate for the job. The inspectors considered this inadequate maintenance procedure a Green NCV violation of Technical Specification 5.4.1.a.
On May 31, 2002, GGNS operations personnel noticed that indications for the RCIC steam flow leakage detection Transmitter 1E31N083B was drifting towards the out of specification reading as indicated on its associated Trip Unit 1E31N683B. To correct
-9-this, GGNS personnel issued MAI 313388 to backfill the transmitter and dispatched instrumentation and control (I&C) personnel to perform the work. These I&C technicians did not realize the process side of the transmitter was at reactor pressure and additionally, the work instructions did not include a step to note system pressures prior to commencing the detector backfill. As a result, the I&C technicians backfilled the transmitter without using a high pressure pump as required when backfilling a detector at reactor pressure. The technicians ended up purging the fluid from the transmitter lines with steam. When the transmitter was restored, fluid condensed in the sensing lines of the transmitter which the transmitter sensed as high steam flow. This made the transmitter effectively detect a steam leak in the RCIC steam line, and by design shut the RCIC steam line isolation Valve E31F063B, thereby rendering the RCIC system inoperable.
The MAI utilized referenced Maintenance Procedure 07-S-13-48, "Filling, Venting, and Equalizing Sensing Lines," Revision 2, which gives generic guidance on how to backfill a differential pressure transmitter for generic backfilling guidance. This maintenance procedure did not provide a means to alert the I&C technicians as to what system pressures were prior to commencing maintenance. Since backfilling this detector normally occurs at off-rated conditions, the procedure was not tuned for the conditions at which it was performed. Such guidance would have provided the I&C technicians proper direction on how to satisfactorily proceed with backfilling this detector without isolating the RCIC system.
This finding is more than minor because the objective of the mitigating systems cornerstone to ensure the availability of systems, including the RCIC system, that respond to initiating events was not totally assured, attributable to inadequate maintenance procedural quality. Using Phase 1 of the SDP, the inspectors determined that this finding represented an actual loss of safety function of the RCIC system and required evaluation using Phase 2 of the SDP. In using Phase 2, the inspectors assumed for SDP purposes that no other mitigating systems were unavailable and the RCIC system was out of service for 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> (less than three days). This analysis resulted in characterizing the finding as Green or of very low safety significance. This determination was made because although the dominating sequences for a loss of the RCIC system are a transient without the power conversion system which utilizes the high pressure core spray system and safety relief valves, and a loss of offsite power which utilizes the emergency diesel generators, these appropriate mitigating systems were available and the unavailability of the RCIC system was of short duration.
The inspectors determined that the failure to prescribe adequate maintenance instructions to check transmitter system pressures to enable proper conduct of backfilling was a violation of Technical Specification 5.4.1, which requires maintenance procedures that can affect the performance of safety-related equipment to be performed in accordance with written instructions appropriate to the circumstances as stated in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. However, this violation is being treated as a NCV (NCV 05000416/2002-004-01) because of the very low safety significance of this condition and because the licensee included this condition in their corrective action program in Condition Report CR-GGN-2002-0947. This condition report documents GGNS personnels efforts to enhance the detector backfill procedure to prevent recurrence of this type of event.
-10-1R20 Refueling and Other Outage Activities (71111.20)
a.
Inspection Scope The inspectors observed refueling outage planning and execution activities. The inspectors review included scheduling, training, outage configuration management, decay heat removal operation and management, reactivity controls, inventory controls, tag out and clearance activities, foreign material exclusion management, and fuel movement and storage. Specific activities observed included:
Reactor scram and shutdown
Reactor cooldown and transition to shutdown cooling
Transition from Mode 3 (hot shutdown) to Mode 4 (cold shutdown)
Shutdown cooling and alternate decay heat removal operations
Operations with potential to drain the reactor vessel during control rod drive mechanism removal and replacement
Drywell inspection closeout activities
Jet Pump 13 removal and replacement
Valve B33 FO67B inspection and repair b.
Findings No findings of significance were identified.
1R22 Surveillance Testing (71111.22)
a.
Inspection Scope The inspectors observed performance of surveillance test procedures and reviewed test data of five selected risk-significant SSCs to assess whether the SSCs satisfied the Technical Specifications, the Updated Final Safety Analysis Report, the Technical Requirements Manual, and licensee procedural requirements; and, to determine if the testing appropriately demonstrated that the SSCs were operationally ready and capable of performing their intended safety functions. The following tests were inspected:
06-CH-1B21-O-0002, "Reactor Coolant Routine Chemistry," Revision 104
06-EL-1L11-Q-0001, "125 Volt Battery Bank All Cell Check," Revision 103
06-OP-1P75-M-0001, "Standby Diesel Generator 11 Functional Test,"
-11-Revision 118
06-OP-1R20-W-0001, Plant AC and DC Electrical Power Distribution Weekly Lineup, Revision 104
06-OP-1T48-M-0001, "Standby Gas Treatment System A Operability,"
Revision 104 b.
Findings No findings of significance were identified.
1R23 Temporary Plant Modifications (71111.23)
a.
Inspection Scope The inspectors reviewed the temporary alteration listed below to assess the following attributes: (1) the adequacy of the safety evaluation; (2) the consistency of the installation with the modification documentation; (3) the updating of drawings and procedures, as applicable; and, (4) the adequacy of the postinstallation testing.
Findings No findings of significance were identified.
1EP6 Drill Observation (71114.06)
a.
Inspection Scope On July 9, 2002, the inspectors observed a planned licensee emergency preparedness quarterly drill. The inspectors reviewed the drill scenario to determine if it reflected realistic plant configurations. The inspectors observed GGNS personnel at various locations during the exercise including the control room simulator, the technical support center, the emergency operations facility, and the operations support center. The inspectors primarily focused on the ability of the emergency response organization to properly classify the simulated emergency through recognition of emergency action levels, their ability to activate the station emergency plan and procedures, and their ability to make proper and timely notifications, as appropriate.
b.
Findings No findings of significance were identified.
-12-3.
SAFEGUARDS Cornerstone: Physical Protection [PP]
3PP3 Response to Contingency Events (71130.03)
The Office of Homeland Security (OHS) developed a Homeland Security Advisory System (HSAS) to disseminate information regarding the risk of terrorist attacks. The HSAS implemented five color-coded threat conditions with a description of corresponding actions at each level. NRC Regulatory Information Summary (RIS) 2002-12a, dated August 19, 2002, NRC Threat Advisory and Protective Measures System, discusses the HSAS and provides additional information on protective measures to licensees.
a.
Inspection Scope On September 10, 2002, the NRC issued a Safeguards Advisory to reactor licensees to implement the protective measures described in RIS 2002-12a in response to the Federal government declaration of threat level orange. Subsequently, on September 24, 2002, the OHS downgraded the national security threat condition to yellow and a corresponding reduction in the risk of a terrorist threat.
The inspectors interviewed licensee personnel and security staff, observed the conduct of security operations, and assessed licensee implementation of the threat level orange protective measures. Inspection results were communicated to the region and headquarters security staff for further evaluation.
b.
Findings No findings of significance were identified.
4.
OTHER ACTIVITIES [OA]
4OA1 Performance Indicator Verification (71151)
a.
Inspection Scope The inspectors verified the accuracy and completeness of the data used to calculate and report performance indicator information for three indicators from the third calendar quarter 2001 through the second calendar quarter 2002. The inspectors used Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline,"
Revision 2, as guidance and interviewed licensee personnel responsible for compiling the information.
- Heat removal system (RCIC system) unavailability
High pressure injection system (high pressure core spray system) unavailability
Safety system functional failures The inspectors also performed routine checks, while on tours throughout the plant, to
-13-ensure that locked high radiation areas were properly secured.
b.
Findings No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
a.
Inspection Scope The inspectors conducted in-depth reviews of the problem identification and resolution aspects of two issues. The inspectors reviewed the GGNS personnels evaluations of operability and reportability for the issues, verified corrective actions were appropriately focused to correct the problems, and that those corrective actions were completed in a manner commensurate with the safety significance of the issue. The scope of the reviews also included determination whether identification was made in a timely manner, whether proper extent of condition was reviewed, and whether the corrective actions were completed in a manner commensurate with safety. The following two issues were reviewed:
Primary containment isolation Valve E12F044A being discovered partially opened on two occasions
Control room air conditioning unit Train B repetitive failures in June and July 2002 The inspectors also reviewed an issue which involved problem identification and resolution causes and documented it as a licensee-identified violation in Section 40A7 of this report.
b.
Findings No other findings of significance were identified.
4OA3 Event Followup (71153)
.1 (Closed) Licensee Event Report 50-416/02-002-00, "RHR System Pressure Higher Than Normal Rendering Primary Containment Isolation Valve (PCIV) Inoperable For About 11 Days" On April 7, 2002, the licensee noted from control room indications that the fill valve for the RHR system from the condensate and refueling water transfer system was not completely shut. Further inspection by the licensee revealed that this valve was also a primary containment isolation valve and had been left in this state for about 11 days.
Based on the indeterminate amount of leakage from the valve in its as-found state, GGNS personnel declared the primary containment isolation valve inoperable. The time period for the declared inoperability was in excess of the allowed outage time set forth in Technical Specification 3.6.1.3, therefore the licensee wrote this licensee event report and the finding was captured in the licensee's corrective action program in Condition
-14-Report CR-GGN-2002-0755.
The inspectors reviewed the licensees safety assessment, condition report corrective actions, and troubleshooting efforts associated with this licensee event report and considered this issue a minor violation of Technical Specification 3.6.1.3.
.2 (Closed) Licensee Event Report 50-416/02-003-00, "Reactor Scram Due To Loss of Service Transformer 21" On June 22, 2002, GGNS received an automatic reactor scram signal and shutdown. A raccoon climbed on the grounding transformer on the 34.5 kV side of Service Transformer 21, one of the two 500 kV dedicated offsite feeder transformers for the site, and created a phase-to-ground current path which actuated protective relays for the transformer that removed the offsite feeder from service. As a result, the main turbine electro-hydraulic control system experienced a dip in pressure which acted to fast close the turbine control valves and scram the reactor. This event was a condition that resulted in automatic actuation of a reactor scram by the reactor protection system, therefore the licensee wrote this licensee event report. In addition, GGNS personnel captured their corrective actions in Condition Reports CR-GGN-2002-1105, CR-GGN-2002-1106, and CR-GGN-2002-1110.
The loss of one of the sites dedicated offsite power feeders represented an increase in plant risk but the inspectors did not identify a performance deficiency pertaining to initiation of the event. Additionally, the inspectors reviewed the reported unexpected system responses, including the failure of the emergency operations facility emergency diesel generator to start, the failure of control room air conditioning system Train B to automatically load on the Division II emergency diesel generator, and the heat up and cool down rate limit violations resulting from the loss and subsequent restart of the reactor recirculation system pumps, and identified no findings of significance associated with these items.
4OA6 Meetings, including Exit On September 19, 2002, the results of the inspection of inservice inspection activities were presented to Mr. W. Eaton, Vice President, Operations, and other members of licensee management.
On October 4, 2002, the resident inspectors presented the inspection results to Mr. and members of his staff.
The inspectors also asked if any materials examined during the inspections should be considered proprietary. No proprietary information was identified by the licensee.
4OA7 Licensee-Identified Violations The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
-15-
10 CFR 50, Appendix B, Criterion XVI states in part that measures shall be established to assure that conditions adverse to quality, such as malfunctions, are promptly identified and corrected. On May 31, 2002, during a monthly surveillance run, the standby gas treatment system Train A enclosure building fan failed to start due to ineffective actions to correct the failure of the fan to start following a previous system outage on May 30, 2002. This condition is described in the licensees corrective action program in Condition Reports CR-GGN-2002-0942 and CR-GGN-2002-0948. Because only the radiological barrier function of the system was degraded, this violation is not more than of very low safety significance, and is being treated as a NCV.
ATTACHMENT PARTIAL LIST OF PERSONS CONTACTED C. Abbott, Quality Assurance Supervisor D. Barfield, Manager, System Engineering R. Barnes, Manager, Training and Development C. Bottemiller, Manager, Plant Licensing K. Christian, Superintendent, Mechanical Maintenance M. Cross, ISI Coordinator, Quality Assurance and Nondestructive Examination W. Deck, Security Superintendent W. Eaton, Vice President, Operations J. Edwards, General Manager, Plant Operations C. Ellsaesser, Manager, Corrective Action and Assessment A. Goel, Senior Engineer, Plant Licensing M. Guynn, Manager, Emergency Preparedness R. Moomaw, Manager, Outage Planning and Scheduling M. Mottsen, Supervisor, Engineering J. Roberts, Director, Nuclear Safety Assurance J. Robertson, Manager, Quality Assurance E. Rogers, Manager, Site Support M. Rohrer, Manager, Maintenance G. Sparks, Manager, Operations D. Watt, Site Welding Engineer, Engineering Programs and Components D. Wiles, Director, Engineering R. Wilson, Superintendent, Radiation Protection H. Yeldell, Manager, Design Engineering ITEMS OPENED, CLOSED, AND DISCUSSED Opened 05000416/2002-004-01 NCV Performance of maintenance using an inadequate procedure leads to isolation of the reactor core cooling isolation system (Section 1R19)
Closed 05000416/2002-002-00 LER RHR system pressure higher than normal rendering primary containment isolation valve (PCIV) inoperable for about 11 days (Section 4OA3)
05000416/2002-003-00 LER Reactor scram due to loss of service Transformer 21 (Section 4OA3)
05000416/2002-004-01 NCV Performance of maintenance using an inadequate procedure leads to isolation of the reactor core cooling isolation (Section 1R19)
-2-LIST OF DOCUMENTS REVIEWED Procedures:
Emergency Plan Procedure 10-S-01-1, "Activation of the Emergency Plan," Revision 109 Emergency Plan Procedure 10-S-01-6, "Notification of Offsite Agencies and Plant On-call Emergency Personnel," Revision 36 Emergency Plan Procedure 10-S-01-33, "Emergency Operations Facility Operations,"
Revision 11 General Maintenance Instruction 07-S-12-44, "Station Battery Pilot Cell Inspection," Revision 11 Grand Gulf Nuclear Station Unit 1 Fire Preplans, Volumes 1 and 2, Revision 11 Off-Normal Event Procedure 05-S-01-EP2, "EP-2A, RPV Control - ATWS," Revision dated April 24, 2001 Off-Normal Event Procedure 05-1-02-VI-1, "Flooding," Revision 102 System Operating Instruction 04-1-01-L11-1, "Plant DC Systems," Revision 115 QAI 9.30, Liquid Penetrant Examination, Revision 5 QAI 9.15, Magnetic Particle Examination, Revision 7 NDE 9.24, Manual Ultrasonic Examination of Reactor Vessel Ligament Areas, Revision 2 NDE 9.26, Ultrasonic Manual Examination of Class 1 Reactor Vessel Welds, Revision 2 NDE 9.23, Ultrasonic Examination of Austenitic Piping Welds, Revision 2 NDE 9.07, Straight Beam Ultrasonic Examination of Bolts and Studs, Revision 2 NDE 9.25, Manual Ultrasonic Examination of Nozzle Radii, Revision 2 NDE 9.04, Ultrasonic Examination of Ferritic Piping Welds, Revision 2 NDE 9.55, Radiographic Examination of ASME, ANSI, AWS, API, AWWA Welds and Components, Revision 0 Condition Reports:
1999-1976 2002-0494 2002-0755 2002-0823 2002-0912 2002-0933 2002-1106 2002-1115 2002-1149 2002-1240 2002-1423 2002-1454
-3-Maintenance Action Items:
250736 304244 307083 308112 308461 310606 312342 313508 314272 315281 317065 317683 318000 318422 318801 319002 319075 Examinations Reviewed:
System Component/Weld Identification Examination Method Reactor Coolant System B13-0910-89 Ultrasonic Examination Reactor Coolant System B13-0904-89 Ultrasonic Examination Reactor Coolant System B13-0909-89 Ultrasonic Examination Feedwater System B21-0746-92 Ultrasonic Examination Feedwater System B21-0433-89 Ultrasonic Examination Feedwater System B21-0442-89 Ultrasonic Examination Feedwater System B21-0452-89 Ultrasonic Examination Feedwater System B21-1078-90 Dye Penetrant Feedwater System B21-0469-89 Ultrasonic Examination Feedwater System B21-0440-89 Magnetic Particle Feedwater System B21-0441-89 Dye Penetrant Feedwater System B21-0349-95 Magnetic Particle Reactor Recirculation B33-1236-92 Ultrasonic Examination Reactor Recirculation B33-1124-92 Ultrasonic Examination Reactor Recirculation B33-0192-89 Dye Penetrant Reactor Recirculation B33-0971-89 Ultrasonic Examination Reactor Recirculation B33-0202-89 Dye Penetrant Control Rod Drive C11-0528-90 Ultrasonic Examination Control Rod Drive C11-0550-90 Ultrasonic Examination
-4-Other Miscellaneous Documents:
Calculation EC-Q1L11-91011, "Station Blackout Evaluation of 125 VDC Division I Battery,"
Revision 0 Calculation EC-Q1L21-90047, "Sizing of 125 VDC Division II Battery and Chargers," Revision 2
"Detroit Diesel Engines Series 149 Service Manual," Revision 4/77 Kohler Generators 500R0ZD Operating Instructions