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Davis-Besse Nuclear Power Station
Davis-Besse Nuclear Power Station
5501 North State Route 2
5501 North State Route 2
Oak Harbor, OH 43449-9760
Oak Harbor, OH 43449-9760
SUBJECT:       DAVIS-BESSE NUCLEAR POWER STATION
SUBJECT:
                NRC SPECIAL TEAM INSPECTION - CORRECTIVE ACTION PROGRAM
DAVIS-BESSE NUCLEAR POWER STATION
                IMPLEMENTATION - REPORT 05000346/2003010(DRS) AND NOTICE of
NRC SPECIAL TEAM INSPECTION - CORRECTIVE ACTION PROGRAM  
                VIOLATION
IMPLEMENTATION - REPORT 05000346/2003010(DRS) AND NOTICE of
VIOLATION
Dear Mr. Myers:
Dear Mr. Myers:
On January 7, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed a special
On January 7, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed a special
corrective action team inspection (CATI) at your Davis-Besse Nuclear Power Station to assess
corrective action team inspection (CATI) at your Davis-Besse Nuclear Power Station to assess
the effectiveness of the implementation of your corrective action program. This inspection
the effectiveness of the implementation of your corrective action program. This inspection
represented a significant input into the NRCs Davis-Besse Oversight Panels (Panel) review of
represented a significant input into the NRCs Davis-Besse Oversight Panels (Panel) review of
Restart Checklist Item 3.a, "Corrective Action Program and also contributed to the Panels
Restart Checklist Item 3.a, "Corrective Action Program and also contributed to the Panels
review of Restart Checklist Items No. 2.c, "Structures, Systems, and Components Inside
review of Restart Checklist Items No. 2.c, "Structures, Systems, and Components Inside
Containment," and 5.b, "Systems Readiness for Restart." The enclosed inspection report
Containment," and 5.b, "Systems Readiness for Restart." The enclosed inspection report
documents the CATI findings which were discussed with you and other members of your staff on
documents the CATI findings which were discussed with you and other members of your staff on
September 9 and November 10, 2003, and on January 7, 2004.
September 9 and November 10, 2003, and on January 7, 2004.
The CATI was accomplished by eleven NRC inspectors and contractors over a period of ten
The CATI was accomplished by eleven NRC inspectors and contractors over a period of ten
months involving five weeks of onsite effort and multiple additional weeks of in-office review.
months involving five weeks of onsite effort and multiple additional weeks of in-office review.  
The CATI evaluated the effectiveness of the implementation of various aspects of your
The CATI evaluated the effectiveness of the implementation of various aspects of your
corrective action program (CAP), including: (1) identifying and documenting plant design-related
corrective action program (CAP), including: (1) identifying and documenting plant design-related
deficiencies; (2) categorizing and prioritizing safety issues for resolution; (3) conducting
deficiencies; (2) categorizing and prioritizing safety issues for resolution; (3) conducting
apparent and root cause analyses; (4) determining extent of condition and (5) implementing
apparent and root cause analyses; (4) determining extent of condition and (5) implementing
appropriate and timely corrective actions to ensure adequate resolution of problems. Overall,
appropriate and timely corrective actions to ensure adequate resolution of problems. Overall,
the CATI team reviewed the resolution of several hundred conditions adverse to quality. Many
the CATI team reviewed the resolution of several hundred conditions adverse to quality. Many
of the deficiencies reviewed by the CATI involved safety system design engineering issues.
of the deficiencies reviewed by the CATI involved safety system design engineering issues.
In addition, the CATI reviewed management involvement in and oversight of the implementation
In addition, the CATI reviewed management involvement in and oversight of the implementation
of the corrective action program, including the routine performance indicators utilized to monitor
of the corrective action program, including the routine performance indicators utilized to monitor
the program implementation, and the effectiveness of conditions adverse to quality trending
the program implementation, and the effectiveness of conditions adverse to quality trending
analyses and quality assessment audits of the CAP implementation. Finally, due to the nature
analyses and quality assessment audits of the CAP implementation. Finally, due to the nature
of multiple NRC inspection findings, the team focused additional effort on assessing the
of multiple NRC inspection findings, the team focused additional effort on assessing the
adequacy of engineering work products, including analyses and calculations.
adequacy of engineering work products, including analyses and calculations.
Notwithstanding a significant number of performance deficiencies identified during the
Notwithstanding a significant number of performance deficiencies identified during the
inspection, based on input from the CATI team, the Panel concluded that the corrective action
inspection, based on input from the CATI team, the Panel concluded that the corrective action
program was sufficiently acceptable for plant restart. The significance of each performance
program was sufficiently acceptable for plant restart. The significance of each performance


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deficiency identified during the inspection was evaluated in accordance with the NRCs
deficiency identified during the inspection was evaluated in accordance with the NRCs
Significance Determination Process and concluded to be of very low safety significance. While
Significance Determination Process and concluded to be of very low safety significance. While
the individual risk significance of each performance deficiency was low, two themes emerged
the individual risk significance of each performance deficiency was low, two themes emerged
from a collective evaluation of the number and nature of the CATI findings:
from a collective evaluation of the number and nature of the CATI findings:
        A weakness in identifying and evaluating the nature and extent of issues when

          performing apparent cause evaluations to identify the cause(s) and full scope of
A weakness in identifying and evaluating the nature and extent of issues when
          necessary corrective actions, particularly in the area of safety system design
performing apparent cause evaluations to identify the cause(s) and full scope of
          deficiencies; and
necessary corrective actions, particularly in the area of safety system design
        A weakness in the quality of engineering work products, including design calculations
deficiencies; and
          and analyses, to correct conditions adverse to quality.

A weakness in the quality of engineering work products, including design calculations
and analyses, to correct conditions adverse to quality.
In addition, the CATI noted that during early part of the extended shutdown of the Davis-Besse
In addition, the CATI noted that during early part of the extended shutdown of the Davis-Besse
facility, you suspended the conditions adverse to quality trending program intended to provide
facility, you suspended the conditions adverse to quality trending program intended to provide
early identification of broader plant equipment and organizational concerns. Your resumption of
early identification of broader plant equipment and organizational concerns. Your resumption of
the trending program was not timely. Further, your corrective action program required the
the trending program was not timely. Further, your corrective action program required the
review of the effectiveness of corrective action taken to address significant conditions adverse
review of the effectiveness of corrective action taken to address significant conditions adverse
to quality six months after implementation of those actions. Sufficient actions had not been
to quality six months after implementation of those actions. Sufficient actions had not been
completed for six months for the CATI to evaluate this area.
completed for six months for the CATI to evaluate this area.
Following the conclusion of the onsite phase of the inspection in September 2003, your staff
Following the conclusion of the onsite phase of the inspection in September 2003, your staff
implemented actions to further assess the specific areas identified by the CATI and develop
implemented actions to further assess the specific areas identified by the CATI and develop
improvement initiatives to address those areas. Those activities were presented publicly to the
improvement initiatives to address those areas. Those activities were presented publicly to the
NRC on November 12, 2003 and discussed further during a public meeting on December 10,
NRC on November 12, 2003 and discussed further during a public meeting on December 10,
2003. Continuing actions to further address the areas of corrective action program
2003. Continuing actions to further address the areas of corrective action program
effectiveness and engineering product quality are documented in your Operational
effectiveness and engineering product quality are documented in your Operational
Improvement Plan, Operating Cycle 14, Revision 3, submitted on February 19, 2003.
Improvement Plan, Operating Cycle 14, Revision 3, submitted on February 19, 2003.
The CATI team has reviewed these ongoing and planned actions and concluded that, if
The CATI team has reviewed these ongoing and planned actions and concluded that, if
properly implemented, they should address the concerns identified during this inspection and
properly implemented, they should address the concerns identified during this inspection and
further improve the corrective action program effectiveness at Davis-Besse. However, the
further improve the corrective action program effectiveness at Davis-Besse. However, the
effectiveness of the actions could not be evaluated by the NRC at this time due to the relatively
effectiveness of the actions could not be evaluated by the NRC at this time due to the relatively
short implementation time of many of those corrective actions.
short implementation time of many of those corrective actions.  
The team noted that, in general, the Nuclear Quality Assurance (NQA) assessments of
The team noted that, in general, the Nuclear Quality Assurance (NQA) assessments of
corrective action program effectiveness identified problems pertaining to corrective action
corrective action program effectiveness identified problems pertaining to corrective action
program implementation that were similar to the issues identified by the CATI. However,
program implementation that were similar to the issues identified by the CATI. However,
resolution of NQAs findings was not sufficiently prompt or effective to address the identified
resolution of NQAs findings was not sufficiently prompt or effective to address the identified
problems and to prevent the underlying deficiencies that led to these NRC findings. Continuing
problems and to prevent the underlying deficiencies that led to these NRC findings. Continuing
diligence by Davis-Besse management will be necessary to assure lasting effective corrective
diligence by Davis-Besse management will be necessary to assure lasting effective corrective
action program implementation. The NRC will continue to closely monitor Davis-Besses
action program implementation. The NRC will continue to closely monitor Davis-Besses
performance to assess the effectiveness of the Davis-Besse corrective actions.
performance to assess the effectiveness of the Davis-Besse corrective actions.
In addition to documenting the results of the CATI, this inspection report documents the closure
In addition to documenting the results of the CATI, this inspection report documents the closure
of Davis-Besse Restart Checklist Items 2.c, "Structures, Systems, and Components Inside
of Davis-Besse Restart Checklist Items 2.c, "Structures, Systems, and Components Inside


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Containment," and 3.a, "Corrective Action Program." Restart checklist item 5.b, Systems
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Containment," and 3.a, "Corrective Action Program." Restart checklist item 5.b, Systems
Readiness for Restart, is not closed in this inspection report.
Readiness for Restart, is not closed in this inspection report.
Based on the results of this inspection, the NRC identified two violations which are cited in the
Based on the results of this inspection, the NRC identified two violations which are cited in the
enclosed Notice of Violation (Notice) and the circumstances surrounding them are described in
enclosed Notice of Violation (Notice) and the circumstances surrounding them are described in
detail in the subject inspection report. The violations are being cited because your staff failed to
detail in the subject inspection report. The violations are being cited because your staff failed to
restore compliance after the violations were identified.
restore compliance after the violations were identified.
Additionally, the NRC identified twenty-six NRC-identified violations of very low safety
Additionally, the NRC identified twenty-six NRC-identified violations of very low safety
significance (Green) and one NRC-identified Severity Level IV violation. These violations are
significance (Green) and one NRC-identified Severity Level IV violation. These violations are
being treated as Non-Cited Violations (NCVs) consistent with Section VI.A of the Enforcement
being treated as Non-Cited Violations (NCVs) consistent with Section VI.A of the Enforcement
Policy. These NCVs are described in the subject inspection report. The violations were
Policy. These NCVs are described in the subject inspection report. The violations were
evaluated in accordance with the "General Statement of Policy and Procedure for NRC
evaluated in accordance with the "General Statement of Policy and Procedure for NRC
Enforcement Actions," (Enforcement Policy), NUREG -1600. The current Enforcement Policy is
Enforcement Actions," (Enforcement Policy), NUREG -1600. The current Enforcement Policy is
included on the NRCs web site at www.nrc.gov; select What we do, Enforcement, then
included on the NRCs web site at www.nrc.gov; select What we do, Enforcement, then
Enforcement Policy.
Enforcement Policy.
You are required to respond to this letter and should follow the instructions specified in the
You are required to respond to this letter and should follow the instructions specified in the
enclosed Notice when preparing your response. The NRC will use your response, in part, to
enclosed Notice when preparing your response. The NRC will use your response, in part, to
determine whether further enforcement action is necessary to ensure compliance with
determine whether further enforcement action is necessary to ensure compliance with
regulatory requirements.
regulatory requirements.
If you contest the severity level or significance of the NCVs described in the report, you should
If you contest the severity level or significance of the NCVs described in the report, you should
also provide a response within 30 days of the date of this inspection report, with the basis for
also provide a response within 30 days of the date of this inspection report, with the basis for
your denial, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
your denial, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, DC 20555-0001, with copies to the Regional Administrator, Region III, 801
Washington, DC 20555-0001, with copies to the Regional Administrator, Region III, 801
Warrenville Road, Suite 255, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S.
Warrenville Road, Suite 255, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S.
Nuclear Regulatory Commission, Washington, DC 20555-001.
Nuclear Regulatory Commission, Washington, DC 20555-001.
Line 129: Line 134:
and its enclosures will be available electronically for public inspection in the NRC Public
and its enclosures will be available electronically for public inspection in the NRC Public
Document Room or from the Publicly Available Records (PARS) component of NRC's
Document Room or from the Publicly Available Records (PARS) component of NRC's
document system (ADAMS). ADAMS is accessible from the NRC Web site at
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


L. Myers                                       -4-
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-4-
To the extent possible, your response should not include any personal privacy, proprietary, or
To the extent possible, your response should not include any personal privacy, proprietary, or
safeguards information so that it can be made available to the Public without redaction.
safeguards information so that it can be made available to the Public without redaction.
                                            Sincerely,
Sincerely,
                                            /RA/
/RA/
                                            John A. Grobe, Chairman
John A. Grobe, Chairman
                                            Davis-Besse Oversight Panel
Davis-Besse Oversight Panel
Docket No. 50-346
Docket No. 50-346
License No. NPF-3
License No. NPF-3
Enclosures:   1. Notice of Violation
Enclosures:
              2. Inspection Report No. 05000346/2003010(DRS)
1. Notice of Violation
cc w/encl:     The Honorable Dennis Kucinich
2. Inspection Report No. 05000346/2003010(DRS)
              G. Leidich, President - FENOC
cc w/encl:
              Plant Manager
The Honorable Dennis Kucinich
              Manager - Regulatory Affairs
G. Leidich, President - FENOC
              M. OReilly, Attorney, FirstEnergy
Plant Manager
              Ohio State Liaison Officer
Manager - Regulatory Affairs
              R. Owen, Administrator, Ohio Department of Health
M. OReilly, Attorney, FirstEnergy
              Public Utilities Commission of Ohio
Ohio State Liaison Officer
              President, Board of County Commissioners
R. Owen, Administrator, Ohio Department of Health
                Of Lucas County
Public Utilities Commission of Ohio
              Steve Arndt, President, Ottawa County Board of Commissioners
President, Board of County Commissioners
              D. Lochbaum, Union Of Concerned Scientists
  Of Lucas County
              J. Riccio, Greenpeace
Steve Arndt, President, Ottawa County Board of Commissioners
              P. Gunter, N.I.R.S.
D. Lochbaum, Union Of Concerned Scientists
J. Riccio, Greenpeace
P. Gunter, N.I.R.S.


L. Myers                                                   -4-
L. Myers
-4-
To the extent possible, your response should not include any personal privacy, proprietary, or
To the extent possible, your response should not include any personal privacy, proprietary, or
safeguards information so that it can be made available to the Public without redaction.
safeguards information so that it can be made available to the Public without redaction.
                                                        Sincerely,
Sincerely,
                                                        /RA/
/RA/
                                                        John A. Grobe, Chairman
John A. Grobe, Chairman
                                                        Davis-Besse Oversight Panel
Davis-Besse Oversight Panel
Docket No. 50-346
Docket No. 50-346
License No. NPF-3
License No. NPF-3
Enclosures:       1. Notice of Violation
Enclosures:
                  2. Inspection Report No. 05000346/2003010(DRS)
1. Notice of Violation
cc w/encl:         The Honorable Dennis Kucinich
2. Inspection Report No. 05000346/2003010(DRS)
                  G. Leidich, President - FENOC
cc w/encl:
                  Plant Manager
The Honorable Dennis Kucinich
                  Manager - Regulatory Affairs
G. Leidich, President - FENOC
                  M. OReilly, Attorney, FirstEnergy
Plant Manager
                  Ohio State Liaison Officer
Manager - Regulatory Affairs
                  R. Owen, Administrator, Ohio Department of Health
M. OReilly, Attorney, FirstEnergy
                  Public Utilities Commission of Ohio
Ohio State Liaison Officer
                  President, Board of County Commissioners
R. Owen, Administrator, Ohio Department of Health
                    Of Lucas County
Public Utilities Commission of Ohio
                  Steve Arndt, President, Ottawa County Board of Commissioners
President, Board of County Commissioners
                  D. Lochbaum, Union Of Concerned Scientists
  Of Lucas County
                  J. Riccio, Greenpeace
Steve Arndt, President, Ottawa County Board of Commissioners
                  P. Gunter, N.I.R.S.
D. Lochbaum, Union Of Concerned Scientists
DOCUMENT NAME: C:\ORPCheckout\FileNET\ML040680070.WPD
J. Riccio, Greenpeace
To receive a copy of this document, indicate in the box: "C" = Copy without enclosure "E"= Copy with enclosure "N"= No copy
P. Gunter, N.I.R.S.
OFFICE       RIII                       RIII                     RIII                       RIII
DOCUMENT NAME: C:\\ORPCheckout\\FileNET\\ML040680070.WPD
NAME         ZFalevits:tr               PLougheed               JLara                     BClayton
To receive a copy of this document, indicate in the box: "C" = Copy without enclosure "E"= Copy with enclosure "N"= No copy
DATE         03/05/04                   did not concur           03/05/04                   03/05/04
OFFICE
OFFICE       RIII                       RIII
RIII
NAME         CLipa                       JGrobe
RIII
DATE         03/05/04                   03/05/04
RIII
                                          OFFICIAL RECORD COPY
RIII
NAME
ZFalevits:tr
PLougheed
JLara
BClayton
DATE
03/05/04
did not concur
03/05/04
03/05/04
OFFICE
RIII
RIII
NAME
CLipa
JGrobe
DATE
03/05/04
03/05/04
OFFICIAL RECORD COPY


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ADAMS Distribution:
ADAMS Distribution:
AJM
AJM
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JRK1
JRK1


Notice of Violation                               -1-
Notice of Violation
                                      NOTICE OF VIOLATION
-1-
First Energy Nuclear Operating Company                                       Docket No. 50-346
NOTICE OF VIOLATION
Davis-Besse Nuclear Power Station                                             License No. NPF-3
First Energy Nuclear Operating Company
                                                                              EA-04-049
Docket No. 50-346
                                                                              EA-04-050
Davis-Besse Nuclear Power Station
License No. NPF-3
EA-04-049
EA-04-050
During an NRC inspection conducted from March 17, 2003 through January 7, 2004, violations
During an NRC inspection conducted from March 17, 2003 through January 7, 2004, violations
of NRC requirements was identified. In accordance with the "General Statement of Policy and
of NRC requirements was identified. In accordance with the "General Statement of Policy and
Procedure for NRC Enforcement Actions," NUREG-1600, the violations are listed below:
Procedure for NRC Enforcement Actions," NUREG-1600, the violations are listed below:
(a)     Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that measures be
(a)
        established to assure that applicable regulatory requirements and the design basis are
Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that measures be
        correctly translated into specifications, drawings, procedures, and instructions. It also
established to assure that applicable regulatory requirements and the design basis are
        requires that measures be provided for verifying or checking the adequacy of design,
correctly translated into specifications, drawings, procedures, and instructions. It also
        such as by the performance of design reviews, by the use of alternate or simplified
requires that measures be provided for verifying or checking the adequacy of design,
        calculational methods, or by the performance of a suitable testing program.
such as by the performance of design reviews, by the use of alternate or simplified
        Contrary to the above, as of August 12, 2003, the licensee failed to verify that the
calculational methods, or by the performance of a suitable testing program.
        design of the service water system discharge path swapover setpoints was adequate.
Contrary to the above, as of August 12, 2003, the licensee failed to verify that the
        Specifically, the analysis performed by the licensee showed that the established
design of the service water system discharge path swapover setpoints was adequate.  
        setpoints were not adequate and the evaluation of the analysis accepted the inadequate
Specifically, the analysis performed by the licensee showed that the established
        setpoint based on non-safety-related equipment performing a safety-related function
setpoints were not adequate and the evaluation of the analysis accepted the inadequate
        under design basis conditions. Neither the analysis nor the evaluation corrected the
setpoint based on non-safety-related equipment performing a safety-related function
        nonconforming condition previously identified in Inspection Report 05000346/2002014.
under design basis conditions. Neither the analysis nor the evaluation corrected the
        This is a violation of very low safety significance (Green).
nonconforming condition previously identified in Inspection Report 05000346/2002014.
(b)     Technical Specification Section 4.05a requires, in part, that the licensee perform
This is a violation of very low safety significance (Green).
        inservice testing of valves in accordance with the ASME OM Code and applicable
(b)
        addenda as required by 10 CFR 50.55a.
Technical Specification Section 4.05a requires, in part, that the licensee perform
        10 CFR 50.55a(f)(4) requires that pumps and valves which are classified as ASME
inservice testing of valves in accordance with the ASME OM Code and applicable
        Code Class 1, 2, and 3 meet the inservice test requirements set forth in the appropriate
addenda as required by 10 CFR 50.55a.
        edition and addenda of the ASME OM Code. It further requires that, during 120-month
10 CFR 50.55a(f)(4) requires that pumps and valves which are classified as ASME
        intervals successive to the initial 120-month interval, tests must comply with the
Code Class 1, 2, and 3 meet the inservice test requirements set forth in the appropriate
        requirements in the latest Code edition and addenda incorporated by reference in
edition and addenda of the ASME OM Code. It further requires that, during 120-month
        paragraph (b) of 10 CFR 50.55a 12 months prior to the start of the 120-month interval.
intervals successive to the initial 120-month interval, tests must comply with the
        Paragraph 50.55a(f)(5)(i) requires that the inservice test program be revised as
requirements in the latest Code edition and addenda incorporated by reference in
        necessary to meet the requirement of paragraph 50.55a(f)(4).
paragraph (b) of 10 CFR 50.55a 12 months prior to the start of the 120-month interval.  
        The ASME OM Code, 1995 edition through the 1996 addenda, Section ISTC 4.5.1
Paragraph 50.55a(f)(5)(i) requires that the inservice test program be revised as
        requires, in part, that check valves be exercised nominally every three months. Section
necessary to meet the requirement of paragraph 50.55a(f)(4).
        ISTC 4.5.4(a) requires, in part, that check valves be exercised by initiating flow and
The ASME OM Code, 1995 edition through the 1996 addenda, Section ISTC 4.5.1
        observing that the obturator traveled to its full open position. Observations shall be
requires, in part, that check valves be exercised nominally every three months. Section
        made by observing a direct indicator (e.g., a position-indicating device) or by other
ISTC 4.5.4(a) requires, in part, that check valves be exercised by initiating flow and
observing that the obturator traveled to its full open position. Observations shall be
made by observing a direct indicator (e.g., a position-indicating device) or by other


Notice of Violation                               -2-
Notice of Violation
        positive means (e.g., changes in system pressure, flow rate, level, temperature, seat
-2-
        leakage, testing, or non-intrusive testing results).
positive means (e.g., changes in system pressure, flow rate, level, temperature, seat
        Contrary to the above, the NRC identified that on September 12, 2003, and other dates,
leakage, testing, or non-intrusive testing results).
        the licensee did not observe by a direct indicator or other positive means that the ASME
Contrary to the above, the NRC identified that on September 12, 2003, and other dates,
        Class 3 service water pump discharge check valve obturator traveled to its full open
the licensee did not observe by a direct indicator or other positive means that the ASME
        position during its quarterly surveillance test. Specifically, on September 12, 2003, the
Class 3 service water pump discharge check valve obturator traveled to its full open
        licensee observed a flow rate of 9718 gpm through valve SW-19, which was less than
position during its quarterly surveillance test. Specifically, on September 12, 2003, the
        the test acceptance criterion of 10,000 gpm, and less than the approximately 10,300
licensee observed a flow rate of 9718 gpm through valve SW-19, which was less than
        gpm used in the licensees most recent accident analysis. Observing flow rates less
the test acceptance criterion of 10,000 gpm, and less than the approximately 10,300
        than required for the valve to perform its safety function was not a positive means to
gpm used in the licensees most recent accident analysis. Observing flow rates less
        determine that the obturator traveled to its full open position and no other direct indicator
than required for the valve to perform its safety function was not a positive means to
        or positive means was used. The NRC approved use of the 1995 Code edition through
determine that the obturator traveled to its full open position and no other direct indicator
        the 1996 addenda for the third inservice testing 120-month interval on March 28, 2003 .
or positive means was used. The NRC approved use of the 1995 Code edition through
        Prior to that date, the licensee was committed to the 1986 Edition (no Addenda) of the
the 1996 addenda for the third inservice testing 120-month interval on March 28, 2003 .  
        ASME Boiler and Pressure Vessel Code, Section XI. The 1986 Code Edition contains
Prior to that date, the licensee was committed to the 1986 Edition (no Addenda) of the
        similar requirements.
ASME Boiler and Pressure Vessel Code, Section XI. The 1986 Code Edition contains
        This is a violation of very low safety significance (Green).
similar requirements.
This is a violation of very low safety significance (Green).
Pursuant to the provisions of 10 CFR 2.201, FirstEnergy Nuclear Operating Company is hereby
Pursuant to the provisions of 10 CFR 2.201, FirstEnergy Nuclear Operating Company is hereby
required to submit a written statement or explanation to the U.S. Nuclear Regulatory
required to submit a written statement or explanation to the U.S. Nuclear Regulatory
Commission, ATTN: Document Control Desk, Washington, DC 20555 with a copy to the
Commission, ATTN: Document Control Desk, Washington, DC 20555 with a copy to the
Regional Administrator, Region III, and a copy to the NRC Resident Inspector at the
Regional Administrator, Region III, and a copy to the NRC Resident Inspector at the
Davis-Besse Nuclear Power Plant, within 30 days of the date of the letter transmitting this
Davis-Besse Nuclear Power Plant, within 30 days of the date of the letter transmitting this
Notice of Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of
Notice of Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of
Violation; EA-04-049 and EA-04-050," and should include for each violation: (1) the reason for
Violation; EA-04-049 and EA-04-050," and should include for each violation: (1) the reason for
the violation, or, if contested, the basis for disputing the violation or severity level; (2) the
the violation, or, if contested, the basis for disputing the violation or severity level; (2) the
corrective steps that have been taken and the results achieved; (3) the corrective steps that will
corrective steps that have been taken and the results achieved; (3) the corrective steps that will
be taken to avoid further violations; and (4) the date when full compliance will be achieved.
be taken to avoid further violations; and (4) the date when full compliance will be achieved.  
Your response may reference or include previous docketed correspondence, if the
Your response may reference or include previous docketed correspondence, if the
correspondence adequately addresses the required response. If an adequate reply is not
correspondence adequately addresses the required response. If an adequate reply is not
received within the time specified in this Notice, an order or a Demand for Information may be
received within the time specified in this Notice, an order or a Demand for Information may be
issued as to why the license should not be modified, suspended, or revoked, or why such other
issued as to why the license should not be modified, suspended, or revoked, or why such other
action as may be proper should not be taken. Where good cause is shown, consideration will
action as may be proper should not be taken. Where good cause is shown, consideration will
be given to extending the response time.
be given to extending the response time.
If you contest this enforcement action, you should also provide a copy of your response, with
If you contest this enforcement action, you should also provide a copy of your response, with
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear
the basis for your denial, to the Director, Office of Enforcement, United States Nuclear
Regulatory Commission, Washington, DC 20555-0001.
Regulatory Commission, Washington, DC 20555-0001.
Because your response will be made available electronically for public inspection in the NRC
Because your response will be made available electronically for public inspection in the NRC
Public Document Room or from the NRCs document system (ADAMS), accessible from the
Public Document Room or from the NRCs document system (ADAMS), accessible from the
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should
NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should
not include any personal privacy, proprietary, or safeguards information so that it can be made
not include any personal privacy, proprietary, or safeguards information so that it can be made
available to the public without redaction. If personal privacy or proprietary information is
available to the public without redaction. If personal privacy or proprietary information is
necessary to provide an acceptable response, then please provide a bracketed copy of your
necessary to provide an acceptable response, then please provide a bracketed copy of your


Notice of Violation                             -3-
Notice of Violation
-3-
response that identifies the information that should be protected and a redacted copy of your
response that identifies the information that should be protected and a redacted copy of your
response that deletes such information. If you request withholding of such material, you must
response that deletes such information. If you request withholding of such material, you must
specifically identify the portions of your response that you seek to have withheld and provide in
specifically identify the portions of your response that you seek to have withheld and provide in
detail the basis for your claim of withholding (e.g., explain why the disclosure of information will
detail the basis for your claim of withholding (e.g., explain why the disclosure of information will
create an unwarranted invasion of personal privacy or provide the information required by
create an unwarranted invasion of personal privacy or provide the information required by
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial
10 CFR 2.390(b) to support a request for withholding confidential commercial or financial
information). If safeguards information is necessary to provide an acceptable response, please
information). If safeguards information is necessary to provide an acceptable response, please
provide the level of protection described in 10 CFR 73.21.
provide the level of protection described in 10 CFR 73.21.
Dated this 5th day of March, 2004
Dated this 5th day of March, 2004


          U.S. NUCLEAR REGULATORY COMMISSION
Enclosure
                          REGION III
U.S. NUCLEAR REGULATORY COMMISSION
Docket No:         50-346
REGION III
License No:         NPF-3
Docket No:
Report No:         05000346/2003010
50-346
Licensee:           FirstEnergy Nuclear Operating Company
License No:
Facility:           Davis-Besse Nuclear Power Station
NPF-3
Location:           5501 North State Route 2
Report No:
                    Oak Harbor, OH 43449
05000346/2003010
Dates:             March 17, 2003 through January 07, 2004
Licensee:
Inspection Team:   Z. Falevits, Lead Senior Reactor Engineering Inspector
FirstEnergy Nuclear Operating Company
                    M. Farber, Senior Reactor Engineering Inspector
Facility:
                    P. Lougheed, Senior Reactor Engineering Inspector
Davis-Besse Nuclear Power Station
                    A. Walker, Senior Reactor Engineering Inspector
Location:
                    D. Chyu, Reactor Engineering Inspector
5501 North State Route 2
                    R. Daley, Reactor Engineering Inspector
Oak Harbor, OH 43449
                    F. Baxter, Electrical Consultant
Dates:
                    W. Bennett, Corrective Action Consultant
March 17, 2003 through January 07, 2004
                    Dr. O. Mazzoni, Electrical Consultant
Inspection Team:
                    J. Panchison, Mechanical Consultant
Z. Falevits, Lead Senior Reactor Engineering Inspector
                    W. Sherbin, Mechanical Consultant
M. Farber, Senior Reactor Engineering Inspector
Approved by:       Julio F. Lara, Chief
P. Lougheed, Senior Reactor Engineering Inspector
                    Electrical Engineering Branch
A. Walker, Senior Reactor Engineering Inspector
                    Division of Reactor Safety
D. Chyu, Reactor Engineering Inspector
                                                                    Enclosure
R. Daley, Reactor Engineering Inspector
F. Baxter, Electrical Consultant
W. Bennett, Corrective Action Consultant
Dr. O. Mazzoni, Electrical Consultant
J. Panchison, Mechanical Consultant
W. Sherbin, Mechanical Consultant
Approved by:
Julio F. Lara, Chief
Electrical Engineering Branch
Division of Reactor Safety


                                          TABLE of CONTENTS
Enclosure
Section                                                                                                                         Page
TABLE of CONTENTS
Section
Page
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
      Inspector-Identified and Self-Revealed Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
Inspector-Identified and Self-Revealed Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
4.     OTHER ACTIVITIES (OA) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
4.
OTHER ACTIVITIES (OA) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
      Background . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
Background . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
      (1)   Corrective Action Program Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . .                       13
(1)
              .1     Adequacy of Licensees Efforts to Identify and Document
Corrective Action Program Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
                    Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .         15
.1
              .2     Adequacy of Licensees Efforts to Categorize and Prioritize
Adequacy of Licensees Efforts to Identify and Document
                    Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .         15
Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
              .3     Adequacy of Licensees Efforts to Evaluate Identified Conditions . . . . .                                     17
.2
              .4     Adequacy of Licensees Efforts to Correct Identified Problems . . . . . .                                     19
Adequacy of Licensees Efforts to Categorize and Prioritize
              .5     Review of Engineering Products and Corrective Actions . . . . . . . . . . .                                   20
Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
              .6     Adequacy of Licensees Efforts to Resolve Procedure Adherence
.3
                    and Quality Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .             20
Adequacy of Licensees Efforts to Evaluate Identified Conditions . . . . . 17
      (2)   Review of the Licensees Internal Assessment Activities . . . . . . . . . . . . . . . . .                             21
.4
              .1     Trending, Self-Assessment, and Evaluation Program
Adequacy of Licensees Efforts to Correct Identified Problems
                    Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .           21
. . . . . . 19
              .2     Corrective Action Program Performance Indicators . . . . . . . . . . . . . . .                                 23
.5
              .3     Nuclear Quality Assessment Audits and Self Assessments of
Review of Engineering Products and Corrective Actions . . . . . . . . . . . 20
                    Corrective Action Program Implementation . . . . . . . . . . . . . . . . . . . . .                             24
.6
      (3)   Management CAP Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
Adequacy of Licensees Efforts to Resolve Procedure Adherence
and Quality Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
(2)
Review of the Licensees Internal Assessment Activities . . . . . . . . . . . . . . . . . 21
.1
Trending, Self-Assessment, and Evaluation Program
Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21
.2
Corrective Action Program Performance Indicators . . . . . . . . . . . . . . . 23
.3
Nuclear Quality Assessment Audits and Self Assessments of
Corrective Action Program Implementation . . . . . . . . . . . . . . . . . . . . . 24
(3)
Management CAP Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
4OA3 Event Response Follow-up - Special Inspection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
4OA3 Event Response Follow-up - Special Inspection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
      (1)   Background . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
(1)
                    Davis-Besse CAP Compliance Review . . . . . . . . . . . . . . . . . . . . . . . . . 27
Background . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
                    Assessment of the Corrective Action Program Compliance Review . . . 27
Davis-Besse CAP Compliance Review . . . . . . . . . . . . . . . . . . . . . . . . . 27
      (2)   Detailed Team Review of Licensee Corrective Actions Implemented to
Assessment of the Corrective Action Program Compliance Review . . . 27
              Address Electrical Issues Previously Identified by NRC or the Licensee . . . . .                                     28
(2)
              .1     Undervoltage Time Delay Relay Setting Did Not Account For
Detailed Team Review of Licensee Corrective Actions Implemented to
                    Instrument Uncertainties . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .               28
Address Electrical Issues Previously Identified by NRC or the Licensee . . . . . 28
              .2     Lack of 480 Vac Class 1E Motor Thermal Overload Protection . . . . . .                                         30
.1
              .3     Failure to Perform Direct Current Contactor Testing to Ensure
Undervoltage Time Delay Relay Setting Did Not Account For
                    Minimum Voltage at Motor Operated Valves . . . . . . . . . . . . . . . . . . . .                               31
Instrument Uncertainties . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
                                                                                                                        Enclosure
.2
Lack of 480 Vac Class 1E Motor Thermal Overload Protection . . . . . . 30
.3
Failure to Perform Direct Current Contactor Testing to Ensure
Minimum Voltage at Motor Operated Valves
. . . . . . . . . . . . . . . . . . . . 31


    .4     Failure to Verify Adequacy of Short Circuit Protection for Direct
Enclosure
          Current Circuits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .     33
ii
    .5     Lack of Calculations to Ensure Minimum Voltage Availability at
.4
          Device Terminals . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       34
Failure to Verify Adequacy of Short Circuit Protection for Direct
    .6     Raychem' Splice Removal on Containment Air Cooler Motor
Current Circuits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33
          Cables . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
.5
    .7     Review of Calculation on the Electric Transient Analysis Profile . . . . . .                             37
Lack of Calculations to Ensure Minimum Voltage Availability at
    .8     Inadequate Grid Voltage Calculations . . . . . . . . . . . . . . . . . . . . . . . . .                   38
Device Terminals . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34
(3) Detailed Team Review of Licensee Corrective Actions Implemented to
.6
    Address Mechanical Issues Previously Identified by NRC or the Licensee . . .                                   38
Raychem' Splice Removal on Containment Air Cooler Motor
    .1     High Pressure Injection Pump Operation Under Long Term
Cables . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
          Minimum Flow . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       39
.7
    .2     Increased Dose Consequences Due to Degraded Thermal
Review of Calculation on the Electric Transient Analysis Profile . . . . . . 37
          Performance Operation of Degraded Containment Air Coolers . . . . . .                                   42
.8
    .3     Containment Air Cooler Air Flow Calculation Concerns . . . . . . . . . . . .                             43
Inadequate Grid Voltage Calculations . . . . . . . . . . . . . . . . . . . . . . . . . 38
    .4     Accumulator Sizing Calculation Errors . . . . . . . . . . . . . . . . . . . . . . . . .                 45
(3)
    .5     Inadequate Blowdown Provisions for Containment Isolation Valve
Detailed Team Review of Licensee Corrective Actions Implemented to
          Accumulators . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .     47
Address Mechanical Issues Previously Identified by NRC or the Licensee
    .6     Non-conservative Calculation Used in Design Analysis to
. . . 38
          Determine Required Service Water Makeup Flow to Component
.1
          Cooling Water . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .     49
High Pressure Injection Pump Operation Under Long Term
    .7     Calculation Concerns for Service Water Pump Room Ventilation
Minimum Flow . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39
          System . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 50
.2
    .8     Inadequate Service Water System Flow Analysis . . . . . . . . . . . . . . . . .                         52
Increased Dose Consequences Due to Degraded Thermal
    .9     Inadequate Flooding Protection for the Service Water System . . . . . .                                 53
Performance Operation of Degraded Containment Air Coolers . . . . . . 42
    .10   Inadequate Service Water System Flow Balance Testing
.3
          Procedure . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 55
Containment Air Cooler Air Flow Calculation Concerns . . . . . . . . . . . . 43
    .11   Service Water Discharge Path Swapover Setpoint . . . . . . . . . . . . . . . .                           56
.4
    .12   Service Water Discharge Check Valve Test Acceptance Criteria . . . . .                                   59
Accumulator Sizing Calculation Errors . . . . . . . . . . . . . . . . . . . . . . . . . 45
    .13   Lack of Design Basis Calculations to Support Service Water
.5
          Single Failure Assumptions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .             61
Inadequate Blowdown Provisions for Containment Isolation Valve
    .14   Auxiliary Feedwater System Calculation Issues With Main Steam
Accumulators . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 47
          Safety Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .   63
.6
    .15   Auxiliary Feedwater Strainer Mesh Size and Preconditioning of
Non-conservative Calculation Used in Design Analysis to
          Auxiliary Feedwater System During Testing . . . . . . . . . . . . . . . . . . . . .                     64
Determine Required Service Water Makeup Flow to Component
    .16   Inadequate Evaluation of System Health Condition Report on Auxiliary
Cooling Water . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 49
          Feedwater Design Bases Calculations . . . . . . . . . . . . . . . . . . . . . . . . .                   67
.7
    .17   Containment Post-LOCA Trisodium Phosphate . . . . . . . . . . . . . . . . . .                           68
Calculation Concerns for Service Water Pump Room Ventilation
    .18   Borated Water Storage Tank Calculation Issues . . . . . . . . . . . . . . . . .                         70
System . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 50
    .19   Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover
.8
          Stud Overstressing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       72
Inadequate Service Water System Flow Analysis . . . . . . . . . . . . . . . . . 52
    .20   Reactor Coolant Pump Inner Gasket Leakage . . . . . . . . . . . . . . . . . . .                         74
.9
    .21   Environmental Qualification of Equipment Not Supported by Analysis
Inadequate Flooding Protection for the Service Water System
            .......................................................                                                 75
. . . . . . 53
    .22   Inadequate Justification for Downgrade of Significant Condition
.10
          Adverse to Quality . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       77
Inadequate Service Water System Flow Balance Testing
    .23   Inappropriate Application of 10 CFR 50.59 . . . . . . . . . . . . . . . . . . . . . .                   78
Procedure . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 55
                                            ii                                                          Enclosure
.11
Service Water Discharge Path Swapover Setpoint . . . . . . . . . . . . . . . . 56
.12
Service Water Discharge Check Valve Test Acceptance Criteria . . . . . 59
.13
Lack of Design Basis Calculations to Support Service Water
Single Failure Assumptions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 61
.14
Auxiliary Feedwater System Calculation Issues With Main Steam
Safety Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 63
.15
Auxiliary Feedwater Strainer Mesh Size and Preconditioning of
Auxiliary Feedwater System During Testing . . . . . . . . . . . . . . . . . . . . . 64
.16
Inadequate Evaluation of System Health Condition Report on Auxiliary
Feedwater Design Bases Calculations . . . . . . . . . . . . . . . . . . . . . . . . . 67
.17
Containment Post-LOCA Trisodium Phosphate . . . . . . . . . . . . . . . . . . 68
.18
Borated Water Storage Tank Calculation Issues . . . . . . . . . . . . . . . . . 70
.19
Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover
Stud Overstressing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 72
.20
Reactor Coolant Pump Inner Gasket Leakage . . . . . . . . . . . . . . . . . . . 74
.21
Environmental Qualification of Equipment Not Supported by Analysis
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 75
.22
Inadequate Justification for Downgrade of Significant Condition
Adverse to Quality . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 77
.23
Inappropriate Application of 10 CFR 50.59 . . . . . . . . . . . . . . . . . . . . . . 78


            .24     Failure to Perform Comprehensive Moderate Energy Line Break
Enclosure
                    Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 81
iii
    (4)   Detailed Team Review of Licensee Corrective Actions Implemented to
.24
            Address Operational Issues Previously Identified by the Licensee . . . . . . . . . . 82
Failure to Perform Comprehensive Moderate Energy Line Break
                    Repetitive Spacer Grid Strap Damage . . . . . . . . . . . . . . . . . . . . . . . . . 82
Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 81
    (5)   Review of Fire Protection Corrective Action Items . . . . . . . . . . . . . . . . . . . . . .                         86
(4)
            .1       Process Monitoring Function for Alternative Shutdown Capability . . . .                                     86
Detailed Team Review of Licensee Corrective Actions Implemented to
            .2       Supporting Functions for Alternative Shutdown Capability . . . . . . . . . .                                 87
Address Operational Issues Previously Identified by the Licensee . . . . . . . . . . 82
            .3       Emergency Diesel Generator Floor Drains Design Deficiency . . . . . . .                                     88
Repetitive Spacer Grid Strap Damage . . . . . . . . . . . . . . . . . . . . . . . . . 82
    (6)   Review of Licensee Event Reports . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .                   89
(5)
            .1       (Discussed) LER 05000346/2002-008-00 and -01: Containment
Review of Fire Protection Corrective Action Items . . . . . . . . . . . . . . . . . . . . . . 86
                    Air Coolers Collective Significance of Degraded Conditions . . . . . . . . .                                 90
.1
            .2       (Closed) LER 05000346/2002-009-00: Degradation of the High
Process Monitoring Function for Alternative Shutdown Capability . . . . 86
                    Pressure Injection Thermal Sleeves . . . . . . . . . . . . . . . . . . . . . . . . . . .                     92
.2
            .3       (Closed) LER 05000346/2003-003-00 and -01: Potential
Supporting Functions for Alternative Shutdown Capability . . . . . . . . . . 87
                    Inadequate High Pressure Injection Pump Minimum Recirculation
.3
                    Flow Following a Small Break Loss of Coolant Accident . . . . . . . . . . .                                 92
Emergency Diesel Generator Floor Drains Design Deficiency . . . . . . . 88
4OA4 Cross-Cutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 94
(6)
Review of Licensee Event Reports
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 89
.1
(Discussed) LER 05000346/2002-008-00 and -01: Containment
Air Coolers Collective Significance of Degraded Conditions . . . . . . . . . 90
.2
(Closed) LER 05000346/2002-009-00: Degradation of the High
Pressure Injection Thermal Sleeves . . . . . . . . . . . . . . . . . . . . . . . . . . . 92
.3
(Closed) LER 05000346/2003-003-00 and -01: Potential
Inadequate High Pressure Injection Pump Minimum Recirculation
Flow Following a Small Break Loss of Coolant Accident
. . . . . . . . . . . 92
4OA4 Cross-Cutting Aspects of Findings
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 94
4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95
4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95
(1) Assessment of the Licensees Corrective Actions to Address Previously Identified
(1)
    Findings Documented in NRC Reports . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95
Assessment of the Licensees Corrective Actions to Address Previously Identified
    .1     Follow up on Findings Documented in Report 05000346/2002012 . . . . . . . . . 95
Findings Documented in NRC Reports . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95
            .1       (Closed) URI 05000346/2002012-02: Potential Impact of
.1
                    Corrosion on the Ground Function of Electrical Conduit in
Follow up on Findings Documented in Report 05000346/2002012 . . . . . . . . . 95
                    Containment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95
.1
            .2       (Closed) URI 05000346/2002012-03: Potential Failure to Follow
(Closed) URI 05000346/2002012-02: Potential Impact of
                    the Procedure for Raychem' Splice Removal on Electrical
Corrosion on the Ground Function of Electrical Conduit in
                    Cables . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 96
Containment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95
    .2     Follow-up on SSDI Findings Documented in Report 05000346/2002014 . . . . .                                           96
.2
            .1       (Discussed) NCV 05000346/2002014-01a: Lack of a Design
(Closed) URI 05000346/2002012-03: Potential Failure to Follow
                    Basis Analysis for Containment Isolation Valve Backup Air
the Procedure for Raychem' Splice Removal on Electrical
                    Supplies . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .     96
Cables . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 96
            .2       (Discussed) NCV 05000346/2002014-01b: Inadequate Blowdown
.2
                    Provisions for Containment Air Cooler Backup Air Accumulators . . . . .                                     96
Follow-up on SSDI Findings Documented in Report 05000346/2002014 . . . . . 96
            .3       (Closed) URI 05000346/2002014-01c: Failure to Perform
.1
                    Comprehensive Moderate Energy Line Break Analysis . . . . . . . . . . . .                                   97
(Discussed) NCV 05000346/2002014-01a: Lack of a Design
            .4       (Closed) URI 05000346/2002014-01d: Lifting of Service Water
Basis Analysis for Containment Isolation Valve Backup Air
                    Relief Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       97
Supplies . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 96
            .5       (Closed) URI 05000346/2002014-01e: Inadequate Service Water
.2
                    Pump Room Temperature Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . .                         97
(Discussed) NCV 05000346/2002014-01b: Inadequate Blowdown
                                                          iii                                                        Enclosure
Provisions for Containment Air Cooler Backup Air Accumulators . . . . . 96
.3
(Closed) URI 05000346/2002014-01c: Failure to Perform
Comprehensive Moderate Energy Line Break Analysis . . . . . . . . . . . . 97
.4
(Closed) URI 05000346/2002014-01d: Lifting of Service Water
Relief Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 97
.5
(Closed) URI 05000346/2002014-01e: Inadequate Service Water
Pump Room Temperature Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . 97


.6 (Closed) URI 05000346/2002014-01f: Inadequate Service Water
Enclosure
    Pump Room Steam Line Break Analysis . . . . . . . . . . . . . . . . . . . . . . . 97
iv
.7 (Closed) URI 05000346/2002014-01g: Inadequate Cable
.6
    Ampacity Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 97
(Closed) URI 05000346/2002014-01f: Inadequate Service Water
.8 (Closed) URI 05000346/2002014-01h: Inadequate Flooding
Pump Room Steam Line Break Analysis . . . . . . . . . . . . . . . . . . . . . . . 97
    Protection for Service Water Pump House . . . . . . . . . . . . . . . . . . . . . . 98
.7
.9 (Discussed) NCV 05000346/2002014-01i: Non-conservative
(Closed) URI 05000346/2002014-01g: Inadequate Cable
    Technical Specification Value for 90 Percent Undervoltage Relays . . . 98
Ampacity Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 97
.10 (Closed) URI 05000346/2002014-01j: Poor Quality Calculation for
.8
    90 Percent Undervoltage Relays . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 98
(Closed) URI 05000346/2002014-01h: Inadequate Flooding
.11 (Discussed) NCV 05000346/2002014-01k: Non-conservative
Protection for Service Water Pump House . . . . . . . . . . . . . . . . . . . . . . 98
    Relay Setpoint Calculation for the 59 Percent Undervoltage
.9
    Relays . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 98
(Discussed) NCV 05000346/2002014-01i: Non-conservative
.12 (Closed) URI 05000346/2002014-01l: Inadequate Calculations for
Technical Specification Value for 90 Percent Undervoltage Relays . . . 98
    Control Room Operator Dose (GDC-19) and Offsite Dose (10
.10
    CFR Part 100) Related to High Pressure Injection Pump Minimum
(Closed) URI 05000346/2002014-01j: Poor Quality Calculation for
    Flow Values . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 99
90 Percent Undervoltage Relays . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 98
.13 (Closed) URI 05000346/2002014-01m: Other GDC-19 and 10
.11
    CFR Part 100 Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 99
(Discussed) NCV 05000346/2002014-01k: Non-conservative
.14 (Closed) URI 05000346/2002014-01n: High Pressure Injection
Relay Setpoint Calculation for the 59 Percent Undervoltage
    Pump Operation Under Long Term Minimum Flow . . . . . . . . . . . . . . . . 99
Relays . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 98
.15 (Closed) URI 05000346/2002014-01o: Some Small Break Loss of
.12
    Coolant Accident Sizes Not Analyzed . . . . . . . . . . . . . . . . . . . . . . . . . . 99
(Closed) URI 05000346/2002014-01l: Inadequate Calculations for
.16 (Closed) URI 05000346/2002014-01p: Inadequate Service Water
Control Room Operator Dose (GDC-19) and Offsite Dose (10
    System Flow Analyses . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
CFR Part 100) Related to High Pressure Injection Pump Minimum
.17 (Closed) URI 05000346/2002014-01q: Inadequate Service Water
Flow Values . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 99
    System Thermal Analyses . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
.13
.18 (Closed) URI 05000346/2002014-01r: Inadequate Ultimate Heat
(Closed) URI 05000346/2002014-01m: Other GDC-19 and 10
    Sink Inventory Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
CFR Part 100 Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 99
.19 (Closed) URI 05000346/2002014-01s: No Valid Service Water
.14
    Pump Net Positive Suction Head Analysis . . . . . . . . . . . . . . . . . . . . . 100
(Closed) URI 05000346/2002014-01n: High Pressure Injection
.20 (Closed) URI 05000346/2002014-01t: Service Water Source
Pump Operation Under Long Term Minimum Flow . . . . . . . . . . . . . . . . 99
    Temperature Analysis for Auxiliary Feedwater . . . . . . . . . . . . . . . . . . 100
.15
.21 (Closed) URI 05000346/2002014-01u: Inadequate Short Circuit
(Closed) URI 05000346/2002014-01o: Some Small Break Loss of
    Calculations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
Coolant Accident Sizes Not Analyzed . . . . . . . . . . . . . . . . . . . . . . . . . . 99
.22 (Discussed) NCV 05000346/2002014-01v: No Analytical Basis for
.16
    Setpoint to Swap Service Water System Discharge Path . . . . . . . . . . 101
(Closed) URI 05000346/2002014-01p: Inadequate Service Water
.23 (Discussed) NCV 05000346/2002014-02a: Service Water
System Flow Analyses . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
    Surveillance Test Did Not Use Worst Case Values . . . . . . . . . . . . . . 101
.17
.24 (Closed) URI 05000346/2002014-02b: Inadequate Service Water
(Closed) URI 05000346/2002014-01q: Inadequate Service Water
    Flow Balance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 101
System Thermal Analyses . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
.25 (Closed) URI 05000346/2002014-03a: Inappropriate Service
.18
    Water Pump Curve Allowable Degradation . . . . . . . . . . . . . . . . . . . . 101
(Closed) URI 05000346/2002014-01r: Inadequate Ultimate Heat
.26 (Closed) URI 05000346/2002014-03b: Repetitive Failures of
Sink Inventory Analysis
    Service Water Relief Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 102
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
.27 (Closed) URI 05000346/2002014-03c: Non-conservative
.19
    Difference in Ultimate Heat Sink Temperature Measurements . . . . . . 102
(Closed) URI 05000346/2002014-01s: No Valid Service Water
                                    iv                                                          Enclosure
Pump Net Positive Suction Head Analysis . . . . . . . . . . . . . . . . . . . . . 100
.20
(Closed) URI 05000346/2002014-01t: Service Water Source
Temperature Analysis for Auxiliary Feedwater . . . . . . . . . . . . . . . . . . 100
.21
(Closed) URI 05000346/2002014-01u: Inadequate Short Circuit
Calculations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100
.22
(Discussed) NCV 05000346/2002014-01v: No Analytical Basis for
Setpoint to Swap Service Water System Discharge Path . . . . . . . . . . 101
.23
(Discussed) NCV 05000346/2002014-02a: Service Water
Surveillance Test Did Not Use Worst Case Values
. . . . . . . . . . . . . . 101
.24
(Closed) URI 05000346/2002014-02b: Inadequate Service Water
Flow Balance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 101
.25
(Closed) URI 05000346/2002014-03a: Inappropriate Service
Water Pump Curve Allowable Degradation
. . . . . . . . . . . . . . . . . . . . 101
.26
(Closed) URI 05000346/2002014-03b: Repetitive Failures of
Service Water Relief Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 102
.27
(Closed) URI 05000346/2002014-03c: Non-conservative
Difference in Ultimate Heat Sink Temperature Measurements . . . . . . 102


            .28   (Discussed) NCV 05000346/2002014-03d: Inadequate Corrective
Enclosure
                  Actions Related to Service Water Pump Discharge Check Valve
v
                  Acceptance Criteria . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       103
.28
            .29   (Closed) URI 05000346/2002014-03e: Non-conservative
(Discussed) NCV 05000346/2002014-03d: Inadequate Corrective
                  Containment Air Cooler Mechanical Stress Analysis . . . . . . . . . . . . .                           103
Actions Related to Service Water Pump Discharge Check Valve
            .30   (Discussed) NCV 05000346/2002014-04: Failure to Perform
Acceptance Criteria . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 103
                  Technical Specification Surveillance for High Pressure Injection
.29
                  Pump Following Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .               103
(Closed) URI 05000346/2002014-03e: Non-conservative
            .31   (Closed) URI 05000346/2002014-05: Question Regarding
Containment Air Cooler Mechanical Stress Analysis . . . . . . . . . . . . . 103
                  Definition of a Passive Failure . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .           104
.30
    .3     Follow-up on SSDI Findings Documented in Report 05000346/2002019 . . . . 104
(Discussed) NCV 05000346/2002014-04: Failure to Perform
                  (Closed) URI 05000346/2002019-031: Final Evaluation of
Technical Specification Surveillance for High Pressure Injection
                  Apparent Cause Evaluation for LER 05000346/2002-006-00 . . . . . . . 104
Pump Following Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 103
    .4     Follow up on Augmented Inspection Team Findings Documented in the
.31
            Cover Letter of Report 05000346/2003016 . . . . . . . . . . . . . . . . . . . . . . . . . .                   104
(Closed) URI 05000346/2002014-05: Question Regarding
            .1     (Discussed) AV 05000346/2003016-01: Technical Specification
Definition of a Passive Failure . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 104
                  Reactor Coolant System Pressure Boundary Leakage . . . . . . . . . . . .                               104
.3
            .2     (Discussed) AV 05000346/2003016-02: Reactor Vessel Head
Follow-up on SSDI Findings Documented in Report 05000346/2002019 . . . . 104
                  Boric Acid Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       105
(Closed) URI 05000346/2002019-031: Final Evaluation of
            .3     (Discussed) AV 05000346/2003016-03: Containment Air Cooler
Apparent Cause Evaluation for LER 05000346/2002-006-00 . . . . . . . 104
                  Boric Acid Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       107
.4
            .4     (Discussed) AV 05000346/2003016-04: Radiation Filter Element
Follow up on Augmented Inspection Team Findings Documented in the
                  Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 107
Cover Letter of Report 05000346/2003016 . . . . . . . . . . . . . . . . . . . . . . . . . . 104
            .5     (Discussed) AV 05000346/2003016-05: Service Structure
.1
                  Modification Delay . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       107
(Discussed) AV 05000346/2003016-01: Technical Specification
            .6     (Discussed) AV 05000346/2003016-06: Reactor Coolant System
Reactor Coolant System Pressure Boundary Leakage . . . . . . . . . . . . 104
                  Unidentified Leakage Trend . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .             109
.2
            .7     (Discussed) AV 05000346/2003016-07: Inadequate Boric Acid
(Discussed) AV 05000346/2003016-02: Reactor Vessel Head
                  Corrosion Control Program Procedure . . . . . . . . . . . . . . . . . . . . . . . .                   110
Boric Acid Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 105
            .8     (Discussed) AV 05000346/2003016-08: Failure to Follow Boric
.3
                  Acid Corrosion Control Program Procedure . . . . . . . . . . . . . . . . . . . .                       110
(Discussed) AV 05000346/2003016-03: Containment Air Cooler
            .9     (Discussed) AV 05000346/2003016-09: Failure to Follow
Boric Acid Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 107
                  Corrective Action Program Procedure . . . . . . . . . . . . . . . . . . . . . . . .                   112
.4
(2) Closure of Restart Checklist Items . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .       112
(Discussed) AV 05000346/2003016-04: Radiation Filter Element
            .1     Restart Checklist Item 2.c: Structures, Systems, and
Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 107
                  Components Inside Containment . . . . . . . . . . . . . . . . . . . . . . . . . . . .                 112
.5
            .2     Restart Checklist Item 3.a: Corrective Action Program . . . . . . . . . . .                           113
(Discussed) AV 05000346/2003016-05: Service Structure
            .3     Restart Checklist Item 5.b: Systems Readiness for Restart . . . . . . .                               113
Modification Delay . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 107
.6
(Discussed) AV 05000346/2003016-06: Reactor Coolant System
Unidentified Leakage Trend . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 109
.7
(Discussed) AV 05000346/2003016-07: Inadequate Boric Acid
Corrosion Control Program Procedure . . . . . . . . . . . . . . . . . . . . . . . . 110
.8
(Discussed) AV 05000346/2003016-08: Failure to Follow Boric
Acid Corrosion Control Program Procedure . . . . . . . . . . . . . . . . . . . . 110
.9
(Discussed) AV 05000346/2003016-09: Failure to Follow
Corrective Action Program Procedure . . . . . . . . . . . . . . . . . . . . . . . . 112
(2)
Closure of Restart Checklist Items
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 112
.1
Restart Checklist Item 2.c: Structures, Systems, and
Components Inside Containment . . . . . . . . . . . . . . . . . . . . . . . . . . . . 112
.2
Restart Checklist Item 3.a: Corrective Action Program . . . . . . . . . . . 113
.3
Restart Checklist Item 5.b: Systems Readiness for Restart
. . . . . . . 113
4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 114
4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 114
            Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 114
Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 114
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A1
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A1
    KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A1
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A1
                                                    v                                                          Enclosure


LIST OF ITEMS OPENED, CLOSED AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . A2
Enclosure
vi
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
. . . . . . . . . . . . . . . . . . . . . A2
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A7
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A7
LIST OF ACRONYMS USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A39
LIST OF ACRONYMS USED
                                    vi                                                          Enclosure
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A39


                                    SUMMARY OF FINDINGS
Enclosure
SUMMARY OF FINDINGS
IR 05000346/2003010(DRS); 03/17/2003 - 01/07/2004; Davis-Besse Nuclear Power Station;
IR 05000346/2003010(DRS); 03/17/2003 - 01/07/2004; Davis-Besse Nuclear Power Station;
Corrective Action Program Implementation Effectiveness
Corrective Action Program Implementation Effectiveness
The inspection consisted of five weeks of on-site activities over a six month period. The
The inspection consisted of five weeks of on-site activities over a six month period. The
specific on-site weeks were the weeks of: March 17, March 31, May 18, August 11, and
specific on-site weeks were the weeks of: March 17, March 31, May 18, August 11, and  
August 25, 2003. This report documents a special corrective action program implementation
August 25, 2003. This report documents a special corrective action program implementation
team inspection. The inspection was conducted to assess the adequacy of the licensees
team inspection. The inspection was conducted to assess the adequacy of the licensees
implementation of the facilitys corrective action program. The inspection was conducted by
implementation of the facilitys corrective action program. The inspection was conducted by
regional engineering inspectors and supplemented by consultants. Two Green findings
regional engineering inspectors and supplemented by consultants. Two Green findings
associated with two cited violations, one Severity Level IV Non-Cited Violation (NCV), and
associated with two cited violations, one Severity Level IV Non-Cited Violation (NCV), and
twenty-six (26) Green findings associated with 26 NCVs were identified.
twenty-six (26) Green findings associated with 26 NCVs were identified.
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
NRC Inspection Manual Chapter 0609, "Significance Determination Process." Findings for
NRC Inspection Manual Chapter 0609, "Significance Determination Process." Findings for
which the significance determination process does not apply may be Green or be assigned a
which the significance determination process does not apply may be Green or be assigned a
severity level after NRC management review. The NRCs program for overseeing the safe
severity level after NRC management review. The NRCs program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
Oversight Process," Revision 3, July 2000.
Oversight Process," Revision 3, July 2000.
A.     Inspector-Identified and Self-Revealed Findings
A.
        Cornerstone: Initiating Events
Inspector-Identified and Self-Revealed Findings
*       Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix R,
Cornerstone: Initiating Events
        Section III.L.2.d, having very low safety significance. Specifically, the licensee failed to
*
        provide the process monitoring function, capable of providing direct readings of the
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix R,
        process variables necessary to perform and control the alternative shutdown, for a
Section III.L.2.d, having very low safety significance. Specifically, the licensee failed to
        control room or cable spreading room fire. Following discovery, the licensee entered the
provide the process monitoring function, capable of providing direct readings of the
        issue into the corrective action program and performed a modification to resolve the
process variables necessary to perform and control the alternative shutdown, for a
        issue. The primary cause of this violation was related to the cross-cutting area of
control room or cable spreading room fire. Following discovery, the licensee entered the
        problem identification and resolution because the licensee had previously identified this
issue into the corrective action program and performed a modification to resolve the
        issue as an enhancement and did not recognize that it was a violation of regulatory
issue. The primary cause of this violation was related to the cross-cutting area of
        requirements.
problem identification and resolution because the licensee had previously identified this
        This issue was more than minor because it affected the initiating events cornerstone
issue as an enhancement and did not recognize that it was a violation of regulatory
        and, by not providing the direct indications necessary for the operators to determine the
requirements.
        status of the idle SG, the probability of experiencing unacceptable stresses on the SG
This issue was more than minor because it affected the initiating events cornerstone
        tubes during the limiting Appendix R scenario was increased. The team determined this
and, by not providing the direct indications necessary for the operators to determine the
        finding to be of very low significance, based upon the low probability of a serious control
status of the idle SG, the probability of experiencing unacceptable stresses on the SG
        room fire combined with the low probability that such a fire would affect this specific
tubes during the limiting Appendix R scenario was increased. The team determined this
        instrumentation detrimentally. Additionally, even in the event that such a fire had
finding to be of very low significance, based upon the low probability of a serious control
        affected this instrumentation, it was likely that the operators still would have been able to
room fire combined with the low probability that such a fire would affect this specific
        prevent these tube stresses through use of manual actions, although this was not a
instrumentation detrimentally. Additionally, even in the event that such a fire had
        credited action in the Fire Protection procedures for this scenario. (Section 4OA3(5)b.1)
affected this instrumentation, it was likely that the operators still would have been able to
                                                                                          Enclosure
prevent these tube stresses through use of manual actions, although this was not a
credited action in the Fire Protection procedures for this scenario. (Section 4OA3(5)b.1)


  Cornerstone: Mitigating Systems
Enclosure
* Green. The team identified a Cited Violation of 10 CFR Part 50, Appendix B,
2
  Criterion III, Design Control. Specifically, the licensee failed to provide a basis for the
Cornerstone: Mitigating Systems
  setpoint to swap the service water system discharge path. This issue was previously
*
  identified as a Non-Cited Violation in Inspection Report 05000346/2002014 and the
Green. The team identified a Cited Violation of 10 CFR Part 50, Appendix B,
  corrective actions taken by the licensee failed to correct the originally identified
Criterion III, Design Control. Specifically, the licensee failed to provide a basis for the
  condition. The primary cause of this violation was related to the cross-cutting areas of
setpoint to swap the service water system discharge path. This issue was previously
  problem identification and resolution and human performance, because the licensee did
identified as a Non-Cited Violation in Inspection Report 05000346/2002014 and the
  not recognize that the corrective actions taken needed to restore compliance with the
corrective actions taken by the licensee failed to correct the originally identified
  identified violation of NRC requirements.
condition. The primary cause of this violation was related to the cross-cutting areas of
  The issue was determined to be more than minor because the licensee had not
problem identification and resolution and human performance, because the licensee did
  corrected a previous violation and was relying on non-safety-related equipment to
not recognize that the corrective actions taken needed to restore compliance with the
  perform a safety function under design bases conditions. Because the issue was
identified violation of NRC requirements.
  previously determined to be of very low safety significance, NRC management
The issue was determined to be more than minor because the licensee had not
  concluded that the violation could be categorized as having very low safety significance.
corrected a previous violation and was relying on non-safety-related equipment to
  (Section 4OA3(3)b.11)
perform a safety function under design bases conditions. Because the issue was
* Green. The team identified a Cited Violation of Technical Specifications Section 4.05a
previously determined to be of very low safety significance, NRC management
  and 10 CFR 50.55a. Specifically, the licensee failed to ensure that the service water
concluded that the violation could be categorized as having very low safety significance.  
  discharge check valve was tested in accordance with the American Society of
(Section 4OA3(3)b.11)
  Mechanical Engineers Code. The primary cause of this violation was related to the
*
  cross-cutting areas of problem identification and resolution and human performance,
Green. The team identified a Cited Violation of Technical Specifications Section 4.05a
  because the licensee did not recognize that the corrective actions taken needed to
and 10 CFR 50.55a. Specifically, the licensee failed to ensure that the service water
  ensure compliance with NRC requirements.
discharge check valve was tested in accordance with the American Society of
  The issue was determined to be more than minor because the inadequate test
Mechanical Engineers Code. The primary cause of this violation was related to the
  acceptance criteria allowed the licensee to accept a check valve as performing its
cross-cutting areas of problem identification and resolution and human performance,
  intended function at less than full system flow. The issue was of very low safety
because the licensee did not recognize that the corrective actions taken needed to
  significance using the Phase 1 of the significance determination process based on the
ensure compliance with NRC requirements.
  licensees determination that the system was operable but degraded.
The issue was determined to be more than minor because the inadequate test
  (Section 4OA3(3)b.12)
acceptance criteria allowed the licensee to accept a check valve as performing its
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
intended function at less than full system flow. The issue was of very low safety
  Criterion III, Design Control, having very low safety significance. Specifically, the
significance using the Phase 1 of the significance determination process based on the
  licensee failed to translate instrument uncertainties into the undervoltage time delay
licensees determination that the system was operable but degraded.
  setting specification for the 4160 Vac buses C1 and D1. Following discovery, the
(Section 4OA3(3)b.12)
  licensee confirmed the settings were acceptable and re-evaluated the potential
*
  temperature effects to the time delay relays.
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  This issue was more than minor because the licensee had to perform calculations to
Criterion III, Design Control, having very low safety significance. Specifically, the
  show that the relays were within their allowable values, and because the licensee
licensee failed to translate instrument uncertainties into the undervoltage time delay
  determined that the increased temperature could cause the time delay to operate
setting specification for the 4160 Vac buses C1 and D1. Following discovery, the
  outside of Technical Specifications limits. The issue was of very low safety significance
licensee confirmed the settings were acceptable and re-evaluated the potential
  using the Phase 1 of the significance determination process since the licensee
temperature effects to the time delay relays.
  considered the instruments to be operable. (Section 4OA3(2)b.1)
This issue was more than minor because the licensee had to perform calculations to
                                            2                                        Enclosure
show that the relays were within their allowable values, and because the licensee
determined that the increased temperature could cause the time delay to operate
outside of Technical Specifications limits. The issue was of very low safety significance
using the Phase 1 of the significance determination process since the licensee
considered the instruments to be operable. (Section 4OA3(2)b.1)


* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
Enclosure
  Criterion III, Design Control, having very low safety significance. Specifically, the
3
  licensee failed to provide motor thermal overload protection for the Class 1E 480
*
  alternating current voltage (Vac) distribution system. Following discovery, the licensee
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  physically modified approximately 53 thermal overload circuits to resolve the
Criterion III, Design Control, having very low safety significance. Specifically, the
  discrepancy. The primary cause of this violation was related to the cross-cutting area of
licensee failed to provide motor thermal overload protection for the Class 1E 480
  human performance because the licensee did not realize the lack of thermal overload
alternating current voltage (Vac) distribution system. Following discovery, the licensee
  protection was an unanalyzed condition and that the station was not in compliance with
physically modified approximately 53 thermal overload circuits to resolve the
  the updated safety analysis report until identified by the team.
discrepancy. The primary cause of this violation was related to the cross-cutting area of
  This issue was more than minor because the licensee failed to ensure that bypassing
human performance because the licensee did not realize the lack of thermal overload
  the thermal overload protection would result in completion of safety functions and
protection was an unanalyzed condition and that the station was not in compliance with
  subsequently had to install thermal overload protection in order to meet the design
the updated safety analysis report until identified by the team.
  requirement. The issue was determined to be of very low safety significance using
This issue was more than minor because the licensee failed to ensure that bypassing
  Phase 1 of the significance determination process because there was reasonable
the thermal overload protection would result in completion of safety functions and
  assurance that the condition did not result in a loss of system function. (Section
subsequently had to install thermal overload protection in order to meet the design
  4OA3(2)b.2)
requirement. The issue was determined to be of very low safety significance using
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
Phase 1 of the significance determination process because there was reasonable
  Criterion XI, Test Control, having very low safety significance. Specifically, the
assurance that the condition did not result in a loss of system function. (Section
  licensee failed to adequately test direct current contactors related to two safety related
4OA3(2)b.2)
  motor operated steam valves associated with the auxiliary feedwater system. Following
*
  discovery, the licensee entered the issue into the corrective action program and was
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  re-evaluating the basis for acceptability of these valves. The primary cause of this
Criterion XI, Test Control, having very low safety significance. Specifically, the
  violation was related to the cross-cutting area of problem identification and resolution
licensee failed to adequately test direct current contactors related to two safety related
  because, although the issue was identified in 2002, the licensee did not see the need to
motor operated steam valves associated with the auxiliary feedwater system. Following
  take corrective action until prompted by the team in 2003.
discovery, the licensee entered the issue into the corrective action program and was  
  This issue was more than minor because the licensee had relied upon an inadequate
re-evaluating the basis for acceptability of these valves. The primary cause of this
  test to show that the contactors were qualified to perform under required conditions and
violation was related to the cross-cutting area of problem identification and resolution
  because the contactors were installed in the plant during previous operating cycles. The
because, although the issue was identified in 2002, the licensee did not see the need to
  issue was of very low safety significance using the Phase 1 of the significance
take corrective action until prompted by the team in 2003.
  determination process because the licensee determined that the valves were operable.
This issue was more than minor because the licensee had relied upon an inadequate
  (Section 4OA3(2)b.3)
test to show that the contactors were qualified to perform under required conditions and
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
because the contactors were installed in the plant during previous operating cycles. The
  Criterion XVI, Corrective Action, having very low safety significance. Specifically, the
issue was of very low safety significance using the Phase 1 of the significance
  licensee failed to identify and correct inadequate short circuit protection for direct current
determination process because the licensee determined that the valves were operable.  
  (DC) circuits. Following discovery, the licensee issued a condition report to document
(Section 4OA3(2)b.3)
  the deficient circuit protection for valves with extremely long circuit lengths. The primary
*
  cause of this violation was related to the cross-cutting area of problem identification and
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  resolution because the licensee had missed several opportunities to identify it as part of
Criterion XVI, Corrective Action, having very low safety significance. Specifically, the
  corrective actions for previously identified DC circuit deficiencies.
licensee failed to identify and correct inadequate short circuit protection for direct current
  This issue was more than minor because the licensee had to perform calculations to
(DC) circuits. Following discovery, the licensee issued a condition report to document
  show that the fuses would adequately protect the equipment and because modifications
the deficient circuit protection for valves with extremely long circuit lengths. The primary
  to those fuses were required. The issue was of very low safety significance using
cause of this violation was related to the cross-cutting area of problem identification and
  Phase 1 of the significance determination process because the licensee concluded the
resolution because the licensee had missed several opportunities to identify it as part of
  equipment was operable. (Section 4OA3(2)b.4)
corrective actions for previously identified DC circuit deficiencies.
                                            3                                        Enclosure
This issue was more than minor because the licensee had to perform calculations to
show that the fuses would adequately protect the equipment and because modifications
to those fuses were required. The issue was of very low safety significance using
Phase 1 of the significance determination process because the licensee concluded the
equipment was operable. (Section 4OA3(2)b.4)


* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
Enclosure
  Criterion III, Design Control, having very low safety significance. Specifically, the
4
  licensee failed to confirm operability of direct current (DC) contactors by ensuring that
*
  minimum voltage was available at the safety related device terminals. The licensee
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  missed several opportunities to correct this design deficiency. Following discovery, the
Criterion III, Design Control, having very low safety significance. Specifically, the
  licensee issued a condition report to evaluate the adequacy of available voltage. The
licensee failed to confirm operability of direct current (DC) contactors by ensuring that
  primary cause of this violation was related to the cross-cutting area of problem
minimum voltage was available at the safety related device terminals. The licensee
  identification and resolution because, although the issue was identified in 2002, the
missed several opportunities to correct this design deficiency. Following discovery, the
  licensee did not see the need to take corrective action until prompted by the team in
licensee issued a condition report to evaluate the adequacy of available voltage. The
  2003.
primary cause of this violation was related to the cross-cutting area of problem
  This issue was more than minor because the licensee had to perform calculations to
identification and resolution because, although the issue was identified in 2002, the
  determine if the devices had sufficient voltage to perform their safety function. The
licensee did not see the need to take corrective action until prompted by the team in
  issue was of very low safety significance using Phase 1 of the significance
2003.
  determination process because the licensee determined that all components were
This issue was more than minor because the licensee had to perform calculations to
  operable. (Section 4OA3(2)b.5)
determine if the devices had sufficient voltage to perform their safety function. The
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
issue was of very low safety significance using Phase 1 of the significance
  Criterion III, Design Control, having very low safety significance. Specifically, the
determination process because the licensee determined that all components were
  licensee failed to verify that the high pressure injection pumps could operate under
operable. (Section 4OA3(2)b.5)
  design basis minimum flow requirements since initial plant startup. The primary cause
*
  of this violation was related to the cross-cutting area of problem identification and
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  resolution because the licensee missed several opportunities to identify and correct the
Criterion III, Design Control, having very low safety significance. Specifically, the
  deficiency.
licensee failed to verify that the high pressure injection pumps could operate under
  This issue was more than minor because the licensee had to perform a test to
design basis minimum flow requirements since initial plant startup. The primary cause
  demonstrate that design basis requirements could be met and because the test results
of this violation was related to the cross-cutting area of problem identification and
  determined that the design basis requirements needed to be changed to ensure that the
resolution because the licensee missed several opportunities to identify and correct the
  HPI pumps could perform their accident required function. The issue was of very low
deficiency.
  safety significance because surveillance test results indicated the lowest flow rate for
This issue was more than minor because the licensee had to perform a test to
  either pump was slightly outside the licensee's new operability band, and therefore, it
demonstrate that design basis requirements could be met and because the test results
  was deemed likely that the pumps would have performed had they been called upon.
determined that the design basis requirements needed to be changed to ensure that the
  The issue screened out of Phase 1 of the significance determination process.
HPI pumps could perform their accident required function. The issue was of very low
  (Section 4OA3(3)b.1)
safety significance because surveillance test results indicated the lowest flow rate for
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
either pump was slightly outside the licensee's new operability band, and therefore, it
  Criterion III, Design Control, having very low safety significance. Specifically, the
was deemed likely that the pumps would have performed had they been called upon.  
  licensee failed to consider worst case minimum pressure differential between service
The issue screened out of Phase 1 of the significance determination process.
  water and component cooling water systems when determining required service water
(Section 4OA3(3)b.1)
  makeup flow to the component cooling water system heat exchangers. Following
*
  discovery, the licensee entered the issue into the corrective action program and
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  performed the necessary calculations. The primary cause of this violation was related to
Criterion III, Design Control, having very low safety significance. Specifically, the
  the cross-cutting area of human performance because the licensee used test data
licensee failed to consider worst case minimum pressure differential between service
  collected during normal operation rather than taking the worst case design conditions
water and component cooling water systems when determining required service water
  and because there was a lack of rigor in the calculation review process.
makeup flow to the component cooling water system heat exchangers. Following
  This issue was more than minor because the licensee needed to perform a new
discovery, the licensee entered the issue into the corrective action program and
  calculation to demonstrate that the service water flow to the component cooling water
performed the necessary calculations. The primary cause of this violation was related to
                                            4                                      Enclosure
the cross-cutting area of human performance because the licensee used test data
collected during normal operation rather than taking the worst case design conditions
and because there was a lack of rigor in the calculation review process.
This issue was more than minor because the licensee needed to perform a new
calculation to demonstrate that the service water flow to the component cooling water


  system was adequate to perform its design function under accident conditions. The
Enclosure
  issue was of very low safety significance because the licensee determined the system
5
  was operable. Therefore, the issue screened out of Phase 1 of the significance
system was adequate to perform its design function under accident conditions. The
  determination process. (Section 4OA3(3)b.6)
issue was of very low safety significance because the licensee determined the system
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
was operable. Therefore, the issue screened out of Phase 1 of the significance
  Criterion III, Design Control, having very low safety significance. Specifically, the
determination process. (Section 4OA3(3)b.6)
  licensee failed to verify the adequacy of the design of the service water (SW) pump
*
  room ventilation system. Following discovery that the design basis calculations were
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  non-conservative, the licensee entered the issue into the corrective action program,
Criterion III, Design Control, having very low safety significance. Specifically, the
  re-performed the calculations, and made appropriate modifications to correct the issues.
licensee failed to verify the adequacy of the design of the service water (SW) pump
  The primary cause of this violation was related to the cross-cutting area of corrective
room ventilation system. Following discovery that the design basis calculations were
  action because the licensee failed to correct all of the originally identified issues until
non-conservative, the licensee entered the issue into the corrective action program,  
  identified by team.
re-performed the calculations, and made appropriate modifications to correct the issues.  
  This issue was more than minor because inadequacies in the calculations resulted in a
The primary cause of this violation was related to the cross-cutting area of corrective
  modification which was required to ensure winter operation was within the allowable
action because the licensee failed to correct all of the originally identified issues until
  temperature range, and because the revised calculation did not include all the summer
identified by team.
  heat loads which could potentially impair the SW pump room ventilation system to
This issue was more than minor because inadequacies in the calculations resulted in a
  perform its safety function. The issue was of very low safety significance because the
modification which was required to ensure winter operation was within the allowable
  licensee determined that past non-procedurally-required compensatory actions had
temperature range, and because the revised calculation did not include all the summer
  prevented the equipment from actually being inoperable. Therefore, the issue screened
heat loads which could potentially impair the SW pump room ventilation system to
  out of Phase 1 of the significance determination process. (Section 4OA3(3)b.7)
perform its safety function. The issue was of very low safety significance because the
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
licensee determined that past non-procedurally-required compensatory actions had
  Criterion III, Design Control, having very low safety significance. Specifically, the
prevented the equipment from actually being inoperable. Therefore, the issue screened
  licensee failed to ensure that the service water system could perform its design function
out of Phase 1 of the significance determination process. (Section 4OA3(3)b.7)
  under all required conditions. Following discovery, the licensee documented the issue in
*
  the corrective action program and performed the necessary calculations.
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  This issue was more than minor because the licensee did not initially have a calculation
Criterion III, Design Control, having very low safety significance. Specifically, the
  which showed that the service water (SW) system could fulfill its design function under
licensee failed to ensure that the service water system could perform its design function
  design basis conditions and because, when the calculation was prepared, it identified
under all required conditions. Following discovery, the licensee documented the issue in
  circumstances where the system would not be able to perform its safety function and
the corrective action program and performed the necessary calculations.
  those circumstances were not evaluated to ensure that the safety function could be met.
This issue was more than minor because the licensee did not initially have a calculation
  The issue was of very low safety significance because the licensee concluded that the
which showed that the service water (SW) system could fulfill its design function under
  SW system had never been unable to perform its safety function. Therefore, the issue
design basis conditions and because, when the calculation was prepared, it identified
  screened out of Phase 1 of the significance determination process.
circumstances where the system would not be able to perform its safety function and
  (Section 4OA3(3)b.8)
those circumstances were not evaluated to ensure that the safety function could be met.  
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
The issue was of very low safety significance because the licensee concluded that the
  Criterion III, Design Control, having very low safety significance. Specifically, the
SW system had never been unable to perform its safety function. Therefore, the issue
  licensee failed to have provisions in place to protect the service water pump room from
screened out of Phase 1 of the significance determination process.  
  flooding. Following discovery, the licensee placed the issue in the corrective action
(Section 4OA3(3)b.8)
  program, evaluated the issue and established procedures to address the issue.
*
  This issue was more than minor because the licensee had to make procedural changes
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  in order to ensure that safety-related equipment was capable of performing its safety
Criterion III, Design Control, having very low safety significance. Specifically, the
  functions. The issue was of very low safety significance because the deficiency only
licensee failed to have provisions in place to protect the service water pump room from
                                            5                                        Enclosure
flooding. Following discovery, the licensee placed the issue in the corrective action
program, evaluated the issue and established procedures to address the issue.
This issue was more than minor because the licensee had to make procedural changes
in order to ensure that safety-related equipment was capable of performing its safety
functions. The issue was of very low safety significance because the deficiency only


  dealt with a lack of procedural guidance. Therefore, the issue screened out of Phase 1
Enclosure
  of the significance determination process. (Section 4OA3(3)b.9)
6
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
dealt with a lack of procedural guidance. Therefore, the issue screened out of Phase 1
  Criterion XI, Test Control, having very low safety significance. Specifically, the
of the significance determination process. (Section 4OA3(3)b.9)
  licensee failed to account for a number of conditions in the service water system flow
*
  balance testing procedures. Following discovery, the licensee placed the issue in the
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  corrective action program, evaluated the issue and established procedures to address
Criterion XI, Test Control, having very low safety significance. Specifically, the
  the issue.
licensee failed to account for a number of conditions in the service water system flow
  This issue was more than minor because procedural changes were necessary in order
balance testing procedures. Following discovery, the licensee placed the issue in the
  to ensure that the safety-related service water (SW) system branch flow rates were
corrective action program, evaluated the issue and established procedures to address
  adequate for the system to perform its safety functions. The issue was of very low
the issue.
  safety significance because the licensee concluded that the system was previously
This issue was more than minor because procedural changes were necessary in order
  capable of meeting its design requirements. Therefore, the issue screened out of
to ensure that the safety-related service water (SW) system branch flow rates were
  Phase 1 of the significance determination process. (Section 4OA3(3)b.10)
adequate for the system to perform its safety functions. The issue was of very low
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
safety significance because the licensee concluded that the system was previously
  Criterion III, Design Control, having very low safety significance. Specifically, the
capable of meeting its design requirements. Therefore, the issue screened out of
  licensee failed to provide an analysis which addressed the service water valve single
Phase 1 of the significance determination process. (Section 4OA3(3)b.10)
  failure assumptions described in the updated safety analysis report. Following
*
  discovery, the licensee entered the issue in the corrective action program. The primary
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  cause of this violation was related to the cross-cutting area of problem identification and
Criterion III, Design Control, having very low safety significance. Specifically, the
  resolution because the licensee had not recognized the impact of the issue on the
licensee failed to provide an analysis which addressed the service water valve single
  design basis and had not corrected it after it was identified in 2002.
failure assumptions described in the updated safety analysis report. Following
  This issue was more than minor because the current calculations were non-conservative
discovery, the licensee entered the issue in the corrective action program. The primary
  and the licensee was not able to show that the service water system could perform its
cause of this violation was related to the cross-cutting area of problem identification and
  safety function under design basis conditions. The issue was of very low safety
resolution because the licensee had not recognized the impact of the issue on the
  significance because the team determined that it was unlikely that the service water
design basis and had not corrected it after it was identified in 2002.
  system would not function during a design basis accident, as there would need to be a
This issue was more than minor because the current calculations were non-conservative
  maximum service water temperature or minimum ultimate heat sink level and a specific
and the licensee was not able to show that the service water system could perform its
  valve single failure. This issue was a design deficiency that would not likely result in the
safety function under design basis conditions. The issue was of very low safety
  loss of function; therefore, the issue screened out of Phase 1 of the significance
significance because the team determined that it was unlikely that the service water
  determination process. (Section 4OA3(3)b.13)
system would not function during a design basis accident, as there would need to be a
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
maximum service water temperature or minimum ultimate heat sink level and a specific
  Criterion III, Design Control, having very low safety significance. Specifically, the
valve single failure. This issue was a design deficiency that would not likely result in the
  licensee failed to ensure that design analyses showed that the auxiliary feedwater
loss of function; therefore, the issue screened out of Phase 1 of the significance
  (AFW) system could perform its safety function under design basis conditions.
determination process. (Section 4OA3(3)b.13)
  Following discovery, the licensee entered the issue into the corrective action program.
*
  The primary cause of this violation was related to the cross-cutting area of human
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  performance, as the licensee used the results of a vendor calculation without verifying
Criterion III, Design Control, having very low safety significance. Specifically, the
  that it was adequate.
licensee failed to ensure that design analyses showed that the auxiliary feedwater
  This issue was more than minor because the calculations were non-conservative and
(AFW) system could perform its safety function under design basis conditions.  
  the calculation of record did not demonstrate that the AFW system could perform its
Following discovery, the licensee entered the issue into the corrective action program.
  safety function under design basis conditions. Based on further analysis, the licensee
The primary cause of this violation was related to the cross-cutting area of human
  concluded the AFW system was operable. Therefore, the issue screened out of
performance, as the licensee used the results of a vendor calculation without verifying
  Phase 1 of the significance determination process and was of very low safety
that it was adequate.
  significance. (Section 4OA3(3)b.14)
This issue was more than minor because the calculations were non-conservative and  
                                            6                                        Enclosure
the calculation of record did not demonstrate that the AFW system could perform its
safety function under design basis conditions. Based on further analysis, the licensee
concluded the AFW system was operable. Therefore, the issue screened out of
Phase 1 of the significance determination process and was of very low safety
significance. (Section 4OA3(3)b.14)


* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
Enclosure
  Criterion XI, Test Control, having very low safety significance. Specifically, the
7
  licensee failed to recognize that flushing the system and blowing down the strainers
*
  upstream of the turbine driven pump bearing cooling water strainers prior to routine
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  surveillances constituted preconditioning of the auxiliary feedwater system. Following
Criterion XI, Test Control, having very low safety significance. Specifically, the
  discovery, the licensee entered the issue into the corrective action program. The
licensee failed to recognize that flushing the system and blowing down the strainers
  primary cause of this violation was related to the cross-cutting area of problem
upstream of the turbine driven pump bearing cooling water strainers prior to routine
  identification and resolution because the licensee had failed to recognize the
surveillances constituted preconditioning of the auxiliary feedwater system. Following
  consequences of the preconditioning when evaluating an earlier issue.
discovery, the licensee entered the issue into the corrective action program. The
  This issue was more than minor because there was not sufficient information to show
primary cause of this violation was related to the cross-cutting area of problem
  that test requirements would have been met had the strainers not been blown down.
identification and resolution because the licensee had failed to recognize the
  The issue was of very low safety significance because the licensee considered the
consequences of the preconditioning when evaluating an earlier issue.
  system operable. Therefore, the issue screened out of Phase 1 of the significance
This issue was more than minor because there was not sufficient information to show
  determination process. (Section 4OA3(3)b.15)
that test requirements would have been met had the strainers not been blown down.  
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
The issue was of very low safety significance because the licensee considered the
  Criterion XVI, Corrective Action, having very low safety significance. Specifically, the
system operable. Therefore, the issue screened out of Phase 1 of the significance
  licensee failed to ensure that emergency core cooling system pump motors were
determination process. (Section 4OA3(3)b.15)
  environmentally qualified for the stated mission time, as stated in a license amendment
*
  request submitted to the NRC. Following discovery, the licensee entered the issue into
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  the corrective action program. The primary cause of this violation was related to the
Criterion XVI, Corrective Action, having very low safety significance. Specifically, the
  cross-cutting area of human performance as the licensee did not ensure that personnel
licensee failed to ensure that emergency core cooling system pump motors were
  developing license documents had the necessary information.
environmentally qualified for the stated mission time, as stated in a license amendment
  This issue was more than minor because, if left uncorrected, this weakness could result
request submitted to the NRC. Following discovery, the licensee entered the issue into
  in a repeat failure of the corrective action program to adequately identify, evaluate and
the corrective action program. The primary cause of this violation was related to the
  correct problems. The issue was of very low safety significance because the licensee
cross-cutting area of human performance as the licensee did not ensure that personnel
  considered that the motors could be environmentally qualified. Therefore, the issue
developing license documents had the necessary information.
  screened out of Phase 1 of the significance determination process.
This issue was more than minor because, if left uncorrected, this weakness could result
  (Section 4OA3(3)b.21)
in a repeat failure of the corrective action program to adequately identify, evaluate and
* Severity Level IV. The team identified a Non-Cited Violation of 10 CFR 50.59,
correct problems. The issue was of very low safety significance because the licensee
  Changes, Tests and Experiments. Specifically, the licensee failed to preform an
considered that the motors could be environmentally qualified. Therefore, the issue
  adequate evaluation of a defacto modification to the plant where the underlying change
screened out of Phase 1 of the significance determination process.
  may have required NRC approval prior to implementation. The design change involved
(Section 4OA3(3)b.21)
  degraded or missing physical barriers that could result in one or more of the diesel
*
  generators failing to fulfill their design function during a tornado. Following discovery,
Severity Level IV. The team identified a Non-Cited Violation of 10 CFR 50.59,
  the licensee entered the issue into the corrective action program and re-performed the
Changes, Tests and Experiments. Specifically, the licensee failed to preform an
  analysis. The licensee also repaired those barriers which were physically degraded.
adequate evaluation of a defacto modification to the plant where the underlying change
  The primary cause of this violation was related to the cross-cutting area of human
may have required NRC approval prior to implementation. The design change involved
  performance as the licensee appeared to selectively choose information from the
degraded or missing physical barriers that could result in one or more of the diesel
  guidance document in order to achieve the desired outcome.
generators failing to fulfill their design function during a tornado. Following discovery,
  Because this issue affected the NRCs ability to perform its regulatory function, this
the licensee entered the issue into the corrective action program and re-performed the
  finding was evaluated with the traditional enforcement process. The finding was
analysis. The licensee also repaired those barriers which were physically degraded.
  determined to be of very low safety significance based on a significance determination
The primary cause of this violation was related to the cross-cutting area of human
                                              7                                    Enclosure
performance as the licensee appeared to selectively choose information from the
guidance document in order to achieve the desired outcome.
Because this issue affected the NRCs ability to perform its regulatory function, this
finding was evaluated with the traditional enforcement process. The finding was
determined to be of very low safety significance based on a significance determination


  process analysis of a loss of offsite power concurrent with loss of one emergency diesel
Enclosure
  generator. (Section 4OA3(3)b.23)
8
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
process analysis of a loss of offsite power concurrent with loss of one emergency diesel
  Criterion III, Design Control, having very low safety significance. Specifically, the
generator. (Section 4OA3(3)b.23)
  licensee failed to include environmental effects of a decay heat removal pump seal
*
  failure in the moderate energy line break analysis. Following discovery, the licensee
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  entered the issue into the corrective action program and re-performed the analysis.
Criterion III, Design Control, having very low safety significance. Specifically, the
  This issue was more than minor because the licensee had to perform calculations to
licensee failed to include environmental effects of a decay heat removal pump seal
  show that the environmental effects were acceptable. The issue was of very low safety
failure in the moderate energy line break analysis. Following discovery, the licensee
  significance because, upon completing the analysis, the licensee determined that the
entered the issue into the corrective action program and re-performed the analysis.
  moderate energy line break heat loads were acceptable and that the system could
This issue was more than minor because the licensee had to perform calculations to
  perform its design function. Therefore, the issue screened out of Phase 1 of the
show that the environmental effects were acceptable. The issue was of very low safety
  significance determination process. (Section 4OA3(3)b.24)
significance because, upon completing the analysis, the licensee determined that the
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Section III.L.2.e,
moderate energy line break heat loads were acceptable and that the system could
  having very low safety significance. Specifically, the licensee failed to provide the
perform its design function. Therefore, the issue screened out of Phase 1 of the
  process cooling and lubrication necessary to permit the operation of the equipment used
significance determination process. (Section 4OA3(3)b.24)
  for safe shutdown functions. Following discovery, the licensee entered the issue into
*
  the corrective action program and performed a modification to resolve the issue. The
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Section III.L.2.e,
  primary cause of this violation was related to the cross-cutting area of problem
having very low safety significance. Specifically, the licensee failed to provide the
  identification and resolution because the licensee had previously identified this issue as
process cooling and lubrication necessary to permit the operation of the equipment used
  an enhancement and did not recognize that it was a violation of regulatory requirements.
for safe shutdown functions. Following discovery, the licensee entered the issue into
  This issue was more than minor because, if left uncorrected, the finding would become
the corrective action program and performed a modification to resolve the issue. The
  a more significant safety concern. By not providing containment air cooling as per the
primary cause of this violation was related to the cross-cutting area of problem
  governing alternative shutdown procedure, the probability of the failure of equipment
identification and resolution because the licensee had previously identified this issue as
  relied upon for safe shutdown was increased. This issue was screened to be of very low
an enhancement and did not recognize that it was a violation of regulatory requirements.
  safety significance because there was not a total loss of safety function for an assumed
This issue was more than minor because, if left uncorrected, the finding would become
  control room fire with evacuation. (Section 4OA3(5)b.2)
a more significant safety concern. By not providing containment air cooling as per the
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50.48(a)(1), having
governing alternative shutdown procedure, the probability of the failure of equipment
  very low safety significance. Specifically, the licensee failed to evaluate the adequacy of
relied upon for safe shutdown was increased. This issue was screened to be of very low
  emergency diesel generator common floor drains following sprinkler system actuation in
safety significance because there was not a total loss of safety function for an assumed
  the fire affected emergency diesel generator room. Following discovery, the licensee
control room fire with evacuation. (Section 4OA3(5)b.2)
  entered the issue into the corrective action program and revised the fire response
*
  procedures to address the issue.
Green. The team identified a Non-Cited Violation of 10 CFR Part 50.48(a)(1), having
  This issue was more than minor because it affected the mitigating systems cornerstone
very low safety significance. Specifically, the licensee failed to evaluate the adequacy of
  and the potential existed that a fire in one emergency diesel generator room would
emergency diesel generator common floor drains following sprinkler system actuation in
  potentially impact the redundant emergency diesel generator following sprinkler actuation
the fire affected emergency diesel generator room. Following discovery, the licensee
  in the fire affected emergency diesel generator room. The finding was of very low safety
entered the issue into the corrective action program and revised the fire response
  significance since this issue was a design deficiency that was confirmed not to result in
procedures to address the issue.
  the loss if function per Generic Letter 91-18, Revision 1. Therefore, the issue screened
This issue was more than minor because it affected the mitigating systems cornerstone
  out of Phase 1 of the significance determination process. (Section 4OA3(5)b.3)
and the potential existed that a fire in one emergency diesel generator room would
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
potentially impact the redundant emergency diesel generator following sprinkler actuation
  Criterion III, Design Control, having very low safety significance. Specifically, the
in the fire affected emergency diesel generator room. The finding was of very low safety
                                            8                                      Enclosure
significance since this issue was a design deficiency that was confirmed not to result in
the loss if function per Generic Letter 91-18, Revision 1. Therefore, the issue screened
out of Phase 1 of the significance determination process. (Section 4OA3(5)b.3)
*
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
Criterion III, Design Control, having very low safety significance. Specifically, the


  licensee failed to provide for the original plant design to incorporate a safety-related
Enclosure
  recirculation path for the high pressure injection (HPI) pumps in the high pressure
9
  recirculation (HPR) mode of operation. Following discovery, the licensee installed an
licensee failed to provide for the original plant design to incorporate a safety-related
  additional minimum flow recirculation line for each HPI pump.
recirculation path for the high pressure injection (HPI) pumps in the high pressure
  This issue was more than minor because the original plant design did not incorporate a
recirculation (HPR) mode of operation. Following discovery, the licensee installed an
  safety-related recirculation path for the HPI pumps in the HPR mode of operation and
additional minimum flow recirculation line for each HPI pump.
  this finding affected the mitigating systems cornerstone. The issue was of very low
This issue was more than minor because the original plant design did not incorporate a
  safety significance because the HPR safety-function would not actually have been lost
safety-related recirculation path for the HPI pumps in the HPR mode of operation and
  because of existing procedure actions for feed and bleed operations in situations where
this finding affected the mitigating systems cornerstone. The issue was of very low
  the steam generators could not be used to remove decay heat. Therefore, the finding
safety significance because the HPR safety-function would not actually have been lost
  screened out as having very low safety significance. Section (4OA3(6)b.3)
because of existing procedure actions for feed and bleed operations in situations where
  Cornerstone: Barrier Integrity
the steam generators could not be used to remove decay heat. Therefore, the finding
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
screened out as having very low safety significance. Section (4OA3(6)b.3)
  Criterion III, Design Control, having very low safety significance. Specifically, the
Cornerstone: Barrier Integrity
  licensee failed to correctly identify and translate the design basis requirements into the
*
  containment air coolers airflow analyses and motor horsepower sizing calculations. The
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  primary cause of this violation was related to the cross-cutting area of problem
Criterion III, Design Control, having very low safety significance. Specifically, the
  identification and resolution as the licensee had previously identified issues with the
licensee failed to correctly identify and translate the design basis requirements into the
  motors, but had not reviewed the design calculation of record. Following discovery, the
containment air coolers airflow analyses and motor horsepower sizing calculations. The
  licensee entered the issue into the corrective action program and performed a new
primary cause of this violation was related to the cross-cutting area of problem
  analysis for the motor.
identification and resolution as the licensee had previously identified issues with the
  This issue was more than minor because the licensee had to revise the associated
motors, but had not reviewed the design calculation of record. Following discovery, the
  calculation to evaluate the existing motor to ensure the containment air coolers (CAC)
licensee entered the issue into the corrective action program and performed a new
  would be able to perform their design function. The issue was evaluated in a Phase 1
analysis for the motor.
  analysis in the significance determination process. Because the issue involved both the
This issue was more than minor because the licensee had to revise the associated
  mitigating system and barrier integrity cornerstones, a Phase 2 analysis was also
calculation to evaluate the existing motor to ensure the containment air coolers (CAC)
  performed. A final evaluation was obtained that the issue was of very low safety
would be able to perform their design function. The issue was evaluated in a Phase 1
  significance. (Section 4OA3(3)b.3)
analysis in the significance determination process. Because the issue involved both the
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
mitigating system and barrier integrity cornerstones, a Phase 2 analysis was also
  Criterion III, Design Control, having very low safety significance. Specifically, the
performed. A final evaluation was obtained that the issue was of very low safety
  licensee failed to evaluate a potential overstressing condition on the reactor coolant
significance. (Section 4OA3(3)b.3)
  pump casing-to-cover studs. Following discovery, the licensee entered the issue into
*
  the corrective action program. The primary cause of this violation was related to the
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  cross-cutting area of problem identification and resolution as the licensee closed a
Criterion III, Design Control, having very low safety significance. Specifically, the
  condition report without recognizing that the apparent condition adverse to quality had
licensee failed to evaluate a potential overstressing condition on the reactor coolant
  not been addressed.
pump casing-to-cover studs. Following discovery, the licensee entered the issue into
  This issue was more than minor because the NRC had to perform calculations to
the corrective action program. The primary cause of this violation was related to the
  determine if the reactor coolant pump studs were within ASME Code allowables. The
cross-cutting area of problem identification and resolution as the licensee closed a
  issue was of very low safety significance based on the NRC determination that the studs
condition report without recognizing that the apparent condition adverse to quality had
  were always functional. Therefore, the issue screened out of the Phase 1 significance
not been addressed.
  determination process as having very low safety significance. (Section 4OA3(3)b.19)
This issue was more than minor because the NRC had to perform calculations to
                                              9                                      Enclosure
determine if the reactor coolant pump studs were within ASME Code allowables. The
issue was of very low safety significance based on the NRC determination that the studs
were always functional. Therefore, the issue screened out of the Phase 1 significance
determination process as having very low safety significance. (Section 4OA3(3)b.19)


* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
Enclosure
  Criterion XVI, Corrective Action, having very low safety significance. Specifically, the
10
  licensee failed to take adequate corrective actions to previous events to prevent
*
  damage to a new fuel assembly spacer grid strap during the final reload of the core in
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  February 2003. Following discovery, the licensee entered the issue into the corrective
Criterion XVI, Corrective Action, having very low safety significance. Specifically, the
  action program. The primary cause of this violation was related to the cross-cutting
licensee failed to take adequate corrective actions to previous events to prevent
  areas of corrective action and human performance, because, despite earlier events, the
damage to a new fuel assembly spacer grid strap during the final reload of the core in
  licensee failed to adequately address the human performance issues that contributed to
February 2003. Following discovery, the licensee entered the issue into the corrective
  this and other fuel spacer grid events.
action program. The primary cause of this violation was related to the cross-cutting
  This issue was more than minor because the licensee failed to prevent recurrence of a
areas of corrective action and human performance, because, despite earlier events, the
  significant condition adverse to quality resulting in damage occurring to previously
licensee failed to adequately address the human performance issues that contributed to
  undamaged fuel assembly grid straps. The issue only involved the fuel barrier and it
this and other fuel spacer grid events.
  screened out of the Phase 1 significance determination process as having very low
This issue was more than minor because the licensee failed to prevent recurrence of a
  safety significance. (Section 4OA3(4)b)
significant condition adverse to quality resulting in damage occurring to previously
  Non-Significance Determination Process Issues
undamaged fuel assembly grid straps. The issue only involved the fuel barrier and it
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
screened out of the Phase 1 significance determination process as having very low
  Criterion III, Design Control, having very low safety significance. Specifically, the
safety significance. (Section 4OA3(4)b)
  licensee failed to assess an increase in the offsite dose to the public following a
Non-Significance Determination Process Issues
  postulated design basis accident due to increased containment pressure. Following
*
  discovery, the licensee entered the issue into the corrective action program and
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  performed the necessary analysis. The primary cause of this violation was related to
Criterion III, Design Control, having very low safety significance. Specifically, the
  the cross-cutting area of problem identification and resolution, because, although the
licensee failed to assess an increase in the offsite dose to the public following a
  issue had been previously identified, the licensee had failed to identify that a revised
postulated design basis accident due to increased containment pressure. Following
  dose assessment was needed until prompted by the NRC.
discovery, the licensee entered the issue into the corrective action program and
  This issue was more than minor because the licensee had to perform calculations to
performed the necessary analysis. The primary cause of this violation was related to
  show that the increased time at higher containment pressures did not result in doses
the cross-cutting area of problem identification and resolution, because, although the
  being above regulatory guide allowables. The mitigating system cornerstone was not
issue had been previously identified, the licensee had failed to identify that a revised
  affected since the finding pertained to offsite dose calculations rather than containment
dose assessment was needed until prompted by the NRC.
  air coolers performance. Based on this review, the team determined that the issue was
This issue was more than minor because the licensee had to perform calculations to
  not covered by any of the revised oversight cornerstones and was, therefore, not
show that the increased time at higher containment pressures did not result in doses
  suitable for SDP analysis. This determination was due to the issue regarded
being above regulatory guide allowables. The mitigating system cornerstone was not
  containment pressure and related to offsite dose consequences. Regional management
affected since the finding pertained to offsite dose calculations rather than containment
  determined that this regulatory issue was of very low safety significance because
air coolers performance. Based on this review, the team determined that the issue was
  projected offsite doses remained less than Regulatory Guide 1.4 allowances.
not covered by any of the revised oversight cornerstones and was, therefore, not
  (Section 4OA3(3)b.2)
suitable for SDP analysis. This determination was due to the issue regarded
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
containment pressure and related to offsite dose consequences. Regional management
  Criterion III, Design Control, having very low safety significance. Specifically, the
determined that this regulatory issue was of very low safety significance because
  licensee failed to implement effective design control measures to check and verify the
projected offsite doses remained less than Regulatory Guide 1.4 allowances.  
  adequacy of the design basis calculation performed for sizing the new accumulators
(Section 4OA3(3)b.2)
  used to hold the service water containment isolation valves closed on a loss of
*
  instrument air. Following discovery, the licensee entered the issue into the corrective
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  action program, revised calculations, and changed the accumulator medium from
Criterion III, Design Control, having very low safety significance. Specifically, the
  compressed air to nitrogen.
licensee failed to implement effective design control measures to check and verify the
                                            10                                      Enclosure
adequacy of the design basis calculation performed for sizing the new accumulators
used to hold the service water containment isolation valves closed on a loss of
instrument air. Following discovery, the licensee entered the issue into the corrective
action program, revised calculations, and changed the accumulator medium from
compressed air to nitrogen.


  This issue was more than minor because the licensee had to change the modification
Enclosure
  design from having accumulators containing pressurized air to accumulators containing
11
  pressurized nitrogen. This finding was evaluated in Phase 1 of the significance
This issue was more than minor because the licensee had to change the modification
  determination process. The mitigating system cornerstone was not affected since the
design from having accumulators containing pressurized air to accumulators containing
  finding pertained to the sizing of accumulators associated with containment isolation
pressurized nitrogen. This finding was evaluated in Phase 1 of the significance
  valves. Therefore, the issue was not covered by any of the revised oversight
determination process. The mitigating system cornerstone was not affected since the
  cornerstones and was, therefore, not suitable for SDP analysis. This determination was
finding pertained to the sizing of accumulators associated with containment isolation
  based on the issue affecting containment isolation valves which provide a barrier to
valves. Therefore, the issue was not covered by any of the revised oversight
  breach of containment and potential offsite dose consequences. Regional management
cornerstones and was, therefore, not suitable for SDP analysis. This determination was
  determined that this regulatory issue was of very low safety significance.
based on the issue affecting containment isolation valves which provide a barrier to
  (Section 4OA3(3)b.4)
breach of containment and potential offsite dose consequences. Regional management
* Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
determined that this regulatory issue was of very low safety significance.
  Criterion III, Design Control, having very low safety significance. Specifically, the
(Section 4OA3(3)b.4)
  licensee failed to translate the postulated radiological consequences of leakage from
*
  engineered safety feature components outside containment into calculations of record
Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,
  for post-accident control room dose and offsite boundary dose. Following discovery, the
Criterion III, Design Control, having very low safety significance. Specifically, the
  licensee entered the issue into the corrective action program and provided a bounding
licensee failed to translate the postulated radiological consequences of leakage from
  evaluation which demonstrated that the increase in dose was within acceptable limits.
engineered safety feature components outside containment into calculations of record
  This issue was more than minor because the licensee had to perform calculations to
for post-accident control room dose and offsite boundary dose. Following discovery, the
  show that the increased doses remained within the post accident dose level
licensee entered the issue into the corrective action program and provided a bounding
  requirements. The issue could not be assessed through the significance determination
evaluation which demonstrated that the increase in dose was within acceptable limits.
  process, because none of the cornerstone objectives addressed design issues dealing
This issue was more than minor because the licensee had to perform calculations to
  with postulated doses following a design basis accident. After determination that the
show that the increased doses remained within the post accident dose level
  increase in dose did not involve an issue requiring a license amendment, Regional
requirements. The issue could not be assessed through the significance determination
  Management concluded the regulatory issue was of very low safety significance.
process, because none of the cornerstone objectives addressed design issues dealing
  (Section 4OA3(3)b.18)
with postulated doses following a design basis accident. After determination that the
B. Licensee-Identified Violations
increase in dose did not involve an issue requiring a license amendment, Regional
  No findings of significance were identified.
Management concluded the regulatory issue was of very low safety significance.  
                                            11                                      Enclosure
(Section 4OA3(3)b.18)
B.
Licensee-Identified Violations
No findings of significance were identified.


                                      REPORT DETAILS
Enclosure
4.   OTHER ACTIVITIES (OA)
12
REPORT DETAILS
4.
OTHER ACTIVITIES (OA)
4OA2 Identification and Resolution of Problems (71152B)
4OA2 Identification and Resolution of Problems (71152B)
    Background
Background
    On March 6, 2002, Davis-Besse personnel notified the NRC of degradation (corrosion)
On March 6, 2002, Davis-Besse personnel notified the NRC of degradation (corrosion)
    of the reactor vessel head material adjacent to a control rod drive mechanism (CRDM)
of the reactor vessel head material adjacent to a control rod drive mechanism (CRDM)
    nozzle. This condition was caused by coolant leakage and boric acid corrosion of the
nozzle. This condition was caused by coolant leakage and boric acid corrosion of the
    head material induced by an undetected crack in the adjacent CRDM nozzle. The
head material induced by an undetected crack in the adjacent CRDM nozzle. The
    degraded area covered in excess of 20 square inches where the low-alloy carbon
degraded area covered in excess of 20 square inches where the low-alloy carbon
    structural steel was corroded away, leaving the thin stainless steel cladding layer. This
structural steel was corroded away, leaving the thin stainless steel cladding layer. This
    condition represented a loss of the reactor vessels pressure retaining design function,
condition represented a loss of the reactor vessels pressure retaining design function,
    since the cladding was not considered as pressure boundary material in the structural
since the cladding was not considered as pressure boundary material in the structural
    design of the reactor pressure vessel. While the cladding did provide a pressure
design of the reactor pressure vessel. While the cladding did provide a pressure
    retaining capability during reactor operations, the identified degradation represented an
retaining capability during reactor operations, the identified degradation represented an
    unacceptable reduction in the margin of safety of one of the three principal fission
unacceptable reduction in the margin of safety of one of the three principal fission
    product barriers at Davis-Besse. This issue was documented in inspection report (IR)
product barriers at Davis-Besse. This issue was documented in inspection report (IR)
    05000346/2002003. The event was captured in the licensee's corrective action program
05000346/2002003. The event was captured in the licensee's corrective action program
    (CAP) as condition report (CR) 02-00891, "Failure to Identify Significant Degradation of
(CAP) as condition report (CR) 02-00891, "Failure to Identify Significant Degradation of
    the Reactor Pressure Vessel Head." The root cause analysis report for the CR
the Reactor Pressure Vessel Head." The root cause analysis report for the CR
    documented that one of the root causes of the event was "less than adequate
documented that one of the root causes of the event was "less than adequate
    implementation of the corrective action program."
implementation of the corrective action program."
    As part of the licensees return to service plan and as corrective action for the
As part of the licensees return to service plan and as corrective action for the
    circumstances that led to the vessel head degradation, the licensee implemented the
circumstances that led to the vessel head degradation, the licensee implemented the
    Davis-Besse system health assurance (SHA) plan. This plan described activities to
Davis-Besse system health assurance (SHA) plan. This plan described activities to
    review plant systems prior to restart to ensure that plant systems were in a condition
review plant systems prior to restart to ensure that plant systems were in a condition
    that would support safe and reliable operation.
that would support safe and reliable operation.
    In an effort to identify adverse trends and problem areas, the licensee performed a
In an effort to identify adverse trends and problem areas, the licensee performed a
    collective review of approximately 600 relatively significant CRs and developed
collective review of approximately 600 relatively significant CRs and developed
    approaches to correct the discrepancies, evaluate the extent of condition, address any
approaches to correct the discrepancies, evaluate the extent of condition, address any
    trends, and resolve the issues. The licensee used a three-phase corrective action
trends, and resolve the issues. The licensee used a three-phase corrective action
    process to identify and resolve deficiencies:
process to identify and resolve deficiencies:
    *       Path A - Resolution of each condition identified and determination of the extent
*
              of condition. This approach used the stations CAP to determine cause, extent
Path A - Resolution of each condition identified and determination of the extent
              of condition, and implement specific corrective actions for discrepancies
of condition. This approach used the stations CAP to determine cause, extent
    *       Path B - Evaluation to provide additional assurance of significant safety function
of condition, and implement specific corrective actions for discrepancies
              capabilities. The collective review identified numerous deficiencies in the areas
*
              of calculations and testing which validated or verified the capability of safety
Path B - Evaluation to provide additional assurance of significant safety function
              systems to perform their functions.
capabilities. The collective review identified numerous deficiencies in the areas
                                                12                                      Enclosure
of calculations and testing which validated or verified the capability of safety
systems to perform their functions.


    *       Path C - Resolution of design-related programmatic issues. The collective
Enclosure
            review identified numerous discrepancies in five design-related programmatic
13
            areas (station flooding, high energy line break, environmental qualification,
*
            seismic qualification, and 10 CFR Part 50, Appendix R - Safe Shutdown) within
Path C - Resolution of design-related programmatic issues. The collective
            each of the five systems selected for a detailed latent issues review. The
review identified numerous discrepancies in five design-related programmatic
            licensee conducted a specific detailed examination of CRs to identify,
areas (station flooding, high energy line break, environmental qualification,
            characterize, determine the extent of condition, and correct the problems in each
seismic qualification, and 10 CFR Part 50, Appendix R - Safe Shutdown) within
            of those programmatic areas.
each of the five systems selected for a detailed latent issues review. The
    The licensees review efforts identified numerous discrepancies involving an inadequate
licensee conducted a specific detailed examination of CRs to identify,
    CAP, inadequate configuration control, degraded hardware conditions, inconsistent and
characterize, determine the extent of condition, and correct the problems in each
    potentially non-conservative assumptions in design basis and licensing basis
of those programmatic areas.
    documents, deficient or unavailable calculations, and non-conservative operating and
The licensees review efforts identified numerous discrepancies involving an inadequate
    test procedures which did not reflect design and licensing basis documents. The
CAP, inadequate configuration control, degraded hardware conditions, inconsistent and
    identified discrepancies were documented in new CRs and these CRs were assessed
potentially non-conservative assumptions in design basis and licensing basis
    for operability impact and significance in accordance with the stations CAP.
documents, deficient or unavailable calculations, and non-conservative operating and
    As part of the NRCs inspection of the SHA plan, a safety system design and
test procedures which did not reflect design and licensing basis documents. The
    performance capability inspection (SSDI) was conducted on three systems: the service
identified discrepancies were documented in new CRs and these CRs were assessed
    water (SW), high pressure injection (HPI), and 4160 volt alternating current (AC)
for operability impact and significance in accordance with the stations CAP.
    electrical distribution systems. This inspection identified numerous deficiencies, which
As part of the NRCs inspection of the SHA plan, a safety system design and
    mirrored the licensee's findings in a number of areas. This inspection, and the resultant
performance capability inspection (SSDI) was conducted on three systems: the service
    findings, were documented in IR 05000346/2002014.
water (SW), high pressure injection (HPI), and 4160 volt alternating current (AC)
(1) Corrective Action Program Implementation
electrical distribution systems. This inspection identified numerous deficiencies, which
a. Inspection Scope
mirrored the licensee's findings in a number of areas. This inspection, and the resultant
    To assess the licensees corrective actions to adequately address the numerous plant
findings, were documented in IR 05000346/2002014.
    deficiencies identified in 2002 during the licensees and NRC reviews, the NRC
(1)
    conducted an in-depth corrective action team inspection (CATI) of the CAP
Corrective Action Program Implementation
    implementation. This inspection was intended to assess the effectiveness of the
  a.
    licensees actions to identify the deficiencies, evaluate the cause(s) and correct the
Inspection Scope
    problems in order to prevent recurrence.
To assess the licensees corrective actions to adequately address the numerous plant
    In order to make the above assessment, the team reviewed selected CRs which
deficiencies identified in 2002 during the licensees and NRC reviews, the NRC
    evaluated the licensees actions to address deficiencies documented in licensee event
conducted an in-depth corrective action team inspection (CATI) of the CAP
    reports (LERs), NRC Non-Cited Violations (NCVs), and NRC unresolved items (URIs)
implementation. This inspection was intended to assess the effectiveness of the
    from previous inspections. The selected CRs also involved issues identified by the
licensees actions to identify the deficiencies, evaluate the cause(s) and correct the
    licensee as part of their system health readiness or latent issue reviews. The team's
problems in order to prevent recurrence.
    focus was on CRs which the licensee had identified as requiring resolution prior to the
In order to make the above assessment, the team reviewed selected CRs which
    restart of the plant, with a further emphasis on those CRs which the licensee had
evaluated the licensees actions to address deficiencies documented in licensee event
    determined to be "significant conditions adverse to quality (SCAQ)."
reports (LERs), NRC Non-Cited Violations (NCVs), and NRC unresolved items (URIs)
    The team specifically assessed the licensee's CAP in four separate areas:
from previous inspections. The selected CRs also involved issues identified by the
    *       Identifying problems; including recognizing performance issues within the CAP
licensee as part of their system health readiness or latent issue reviews. The team's
            itself;
focus was on CRs which the licensee had identified as requiring resolution prior to the
                                              13                                      Enclosure
restart of the plant, with a further emphasis on those CRs which the licensee had
determined to be "significant conditions adverse to quality (SCAQ)."
The team specifically assessed the licensee's CAP in four separate areas:
*
Identifying problems; including recognizing performance issues within the CAP
itself;


  *       Categorizing and prioritizing problems, with a specific emphasis on the licensee's
Enclosure
            use of a process termed as "rollovers";
14
  *       Evaluating those problems; including assessing root and apparent causes,
*
            extent of conditions, operability and reportability;
Categorizing and prioritizing problems, with a specific emphasis on the licensee's
  *       Correcting problems, including not only the originally identified problem but any
use of a process termed as "rollovers";
            issues identified as part of the evaluation, assessment of effectiveness of the
*
            corrective actions and actions taken to prevent recurrence.
Evaluating those problems; including assessing root and apparent causes,
  In addition, the team assessed two areas where a number of problems were identified.
extent of conditions, operability and reportability;
  These were:
*
  *       Engineering Resolution of Design Deficiencies and
Correcting problems, including not only the originally identified problem but any
  *       Procedure Quality and Adherence
issues identified as part of the evaluation, assessment of effectiveness of the
b. Observations and Findings
corrective actions and actions taken to prevent recurrence.
  The corrective action program was described in procedure NOP-LP-2001, "Condition
In addition, the team assessed two areas where a number of problems were identified.  
  Report Process." This procedure was significantly revised in March 2003, and again in
These were:
  May 2003. The CAP consisted of a process to identify and resolve potential adverse or
*
  undesirable conditions. It included issues, concerns, observations, equipment
Engineering Resolution of Design Deficiencies and
  deficiencies, human performance problems, equipment failures and programmatic
*
  deficiencies.
Procedure Quality and Adherence
  The team began its inspection in March 2003. However, due to the licensee not being
  b.
  ready for the inspection at that time, the inspection was delayed until May 2003, and the
Observations and Findings
  most effective inspection actually occurred in August 2003, when the licensee had
The corrective action program was described in procedure NOP-LP-2001, "Condition
  completed sufficient packages for the team to review.
Report Process." This procedure was significantly revised in March 2003, and again in
  As described below, at the conclusion of the inspection, the team determined that,
May 2003. The CAP consisted of a process to identify and resolve potential adverse or
  overall, the licensee's program for identifying, prioritizing, evaluating, and correcting
undesirable conditions. It included issues, concerns, observations, equipment
  performance deficiencies was acceptable. However, the team also observed that the
deficiencies, human performance problems, equipment failures and programmatic
  licensees actions to identify non-conforming issues and prevent recurrence were often
deficiencies.
  minimally effective. The team also identified evaluations which were narrowly focused
The team began its inspection in March 2003. However, due to the licensee not being
  and not probing in nature. Consequently, the resulting corrective actions were also
ready for the inspection at that time, the inspection was delayed until May 2003, and the
  narrowly focused. In areas where the licensee had established corrective actions, the
most effective inspection actually occurred in August 2003, when the licensee had
  effectiveness of these actions could not be readily determined at the end of the
completed sufficient packages for the team to review.
  inspection due to the short time frame since implementation.
As described below, at the conclusion of the inspection, the team determined that,
  During the inspection, the team reviewed approximately 150 CRs. Of these, the team
overall, the licensee's program for identifying, prioritizing, evaluating, and correcting
  determined that approximately 120 had weaknesses or deficiencies, of some type. As a
performance deficiencies was acceptable. However, the team also observed that the
  result of the teams findings, the licensee initiated approximately 120 additional CRs to
licensees actions to identify non-conforming issues and prevent recurrence were often
  document and address the teams findings. Overall, the team determined that
minimally effective. The team also identified evaluations which were narrowly focused
  approximately 80 percent of the CRs actually reviewed by the team had weaknesses or
and not probing in nature. Consequently, the resulting corrective actions were also
  deficiencies to some degree. The weaknesses and deficiencies identified by the team
narrowly focused. In areas where the licensee had established corrective actions, the
  resulted in the identification of findings documented in this inspection report.
effectiveness of these actions could not be readily determined at the end of the
  Subsequent to the onsite inspection, on November 12 and December 10, 2003, the
inspection due to the short time frame since implementation.
  licensee presented to the NRC, the planned actions to address the issues and concerns
During the inspection, the team reviewed approximately 150 CRs. Of these, the team
  identified by the CATI. As part of these meetings, the licensee made a number of
determined that approximately 120 had weaknesses or deficiencies, of some type. As a
                                              14                                      Enclosure
result of the teams findings, the licensee initiated approximately 120 additional CRs to
document and address the teams findings. Overall, the team determined that
approximately 80 percent of the CRs actually reviewed by the team had weaknesses or
deficiencies to some degree. The weaknesses and deficiencies identified by the team
resulted in the identification of findings documented in this inspection report.
Subsequent to the onsite inspection, on November 12 and December 10, 2003, the
licensee presented to the NRC, the planned actions to address the issues and concerns
identified by the CATI. As part of these meetings, the licensee made a number of


  commitments to further improve the CAP as part of its Operational Improvement Plan
Enclosure
  for Cycle 14, Revision 3. The team recognized that the improvement plan described
15
  actions that should address the teams areas of concerns. Additionally, the licensee
commitments to further improve the CAP as part of its Operational Improvement Plan
  implemented some improvements in the CAP. Examples included the revised CAP
for Cycle 14, Revision 3. The team recognized that the improvement plan described
  procedure and the newly established CR analyst positions.
actions that should address the teams areas of concerns. Additionally, the licensee
.1 Adequacy of Licensee's Efforts to Identify and Document Problems
implemented some improvements in the CAP. Examples included the revised CAP
  The team determined that the licensee, overall, was adequately identifying and
procedure and the newly established CR analyst positions.
  documenting problems. However, a number of examples were identified where the
    .1
  licensee had failed to identify or to document problems, particularly in the area of
Adequacy of Licensee's Efforts to Identify and Document Problems
  design-related deficiencies. The team attributed these issues to a lack of attention to
The team determined that the licensee, overall, was adequately identifying and
  detail, weak knowledge of system design basis, and a failure to follow CAP procedures.
documenting problems. However, a number of examples were identified where the
  Specific examples are listed below, and the more significant ones are discussed in
licensee had failed to identify or to document problems, particularly in the area of
  Sections 4OA3(2) and 4OA3(3) of this report.
design-related deficiencies. The team attributed these issues to a lack of attention to
  *       Failure to identify the lack of thermal overload protection for safety related
detail, weak knowledge of system design basis, and a failure to follow CAP procedures.  
          motors (See Section 4OA3(2)b.2 for additional details);
Specific examples are listed below, and the more significant ones are discussed in
  *       Failure to identify oversized fuses in safety related motor operated circuits (See
Sections 4OA3(2) and 4OA3(3) of this report.
          Section 4OA3(2)b.4 for additional details);
*
  *       Failure to identify the main steam safety valve (MSSV) setpoint drift and
Failure to identify the lack of thermal overload protection for safety related
          accumulation, and the potential affect on auxiliary feedwater (AFW) pump flow
motors (See Section 4OA3(2)b.2 for additional details);
          (See Section 4OA3(3)b.14 for additional details);
*
  *       Failure to identify potential design problems with the containment air coolers
Failure to identify oversized fuses in safety related motor operated circuits (See
          (CACs) (See Sections 4OA3(3)b.2 and 4OA3(3)b.3 for additional details);
Section 4OA3(2)b.4 for additional details);
  *       Failure to write a CR for SW calculational deficiencies. (See CR 03-03977);
*
  *       Failure to generate a CR to address a problem identified during the SSDI and
Failure to identify the main steam safety valve (MSSV) setpoint drift and
          which was documented in that IR as NCV 02-014-01b (See Section 4OA3(3)b.5
accumulation, and the potential affect on auxiliary feedwater (AFW) pump flow
          for additional details);
(See Section 4OA3(3)b.14 for additional details);
  *       Failure to identify lack of breaker coordination (CR 03-03572); and
*
  *       Failure to identify configuration control discrepancies (CR 03-02699).
Failure to identify potential design problems with the containment air coolers
.2 Adequacy of Licensee's Efforts to Categorize and Prioritize Problems
(CACs) (See Sections 4OA3(3)b.2 and 4OA3(3)b.3 for additional details);
  The team determined that the licensee, overall, was adequately categorizing items in
*
  regard to their safety significance and impact upon plant operation. The licensee also
Failure to write a CR for SW calculational deficiencies. (See CR 03-03977);
  generally appeared to be assigning an appropriate priority both to performing evaluations
*
  and completing corrective actions prior to restart of the plant.
Failure to generate a CR to address a problem identified during the SSDI and
  However, early in the inspections the team did identify a concern with a process the
which was documented in that IR as NCV 02-014-01b (See Section 4OA3(3)b.5
  licensee was using as part of their categorization process. This process, referred to as
for additional details);
  "rollovers, allowed the licensee to disposition CRs by transferring either a portion or the
*
                                              15                                      Enclosure
Failure to identify lack of breaker coordination (CR 03-03572); and
*
Failure to identify configuration control discrepancies (CR 03-02699).
    .2
Adequacy of Licensee's Efforts to Categorize and Prioritize Problems
The team determined that the licensee, overall, was adequately categorizing items in
regard to their safety significance and impact upon plant operation. The licensee also
generally appeared to be assigning an appropriate priority both to performing evaluations
and completing corrective actions prior to restart of the plant.
However, early in the inspections the team did identify a concern with a process the
licensee was using as part of their categorization process. This process, referred to as
"rollovers, allowed the licensee to disposition CRs by transferring either a portion or the


entire issue to one or more additional other open CRs. The licensee did place a
Enclosure
16
entire issue to one or more additional other open CRs. The licensee did place a
condition that the "rolled-into" CRs had to be of equal or greater category and had to
condition that the "rolled-into" CRs had to be of equal or greater category and had to
address the same issues. However, the issues described in the "rolled-out-of" CRs could
address the same issues. However, the issues described in the "rolled-out-of" CRs could
be broken into several different "rolled-into" CRs and "rolling" could occur on multiple
be broken into several different "rolled-into" CRs and "rolling" could occur on multiple
occasions (i.e., CR 1 was rolled into CR 2 which was rolled into CR 3, which then rolled
occasions (i.e., CR 1 was rolled into CR 2 which was rolled into CR 3, which then rolled
out part of CR 1s issues to CR 4...). This was especially true in regard to specified
out part of CR 1s issues to CR 4...). This was especially true in regard to specified
corrective actions. As an example, the team identified that more than 25 corrective
corrective actions. As an example, the team identified that more than 25 corrective
actions were rolled over into CRs 02-00891, "Failure to Identify Significant Degradation of
actions were rolled over into CRs 02-00891, "Failure to Identify Significant Degradation of
the Reactor Pressure Vessel Head," and CR 02-04884, "Ineffective Corrective Action
the Reactor Pressure Vessel Head," and CR 02-04884, "Ineffective Corrective Action
Problem Resolution." Some problems were identified, and the extent of the rollover
Problem Resolution." Some problems were identified, and the extent of the rollover
process early in the inspection made it extremely difficult for the team to accurately
process early in the inspection made it extremely difficult for the team to accurately
assess whether the overall process was adequately controlled and that corrective actions
assess whether the overall process was adequately controlled and that corrective actions
were effectively implemented.
were effectively implemented.
The team also noted that the CAP defined that a CR should only be listed as "closed"
The team also noted that the CAP defined that a CR should only be listed as "closed"
when the evaluation was completed and all corrective actions were implemented.
when the evaluation was completed and all corrective actions were implemented.  
However, the licensee frequently classified a "rolled out of" CR as "Closed", because the
However, the licensee frequently classified a "rolled out of" CR as "Closed", because the
evaluation and/or the corrective actions were transferred to another CR. This gave a
evaluation and/or the corrective actions were transferred to another CR. This gave a
somewhat artificial characterization as to the status of resolution of identified issues.
somewhat artificial characterization as to the status of resolution of identified issues.  
The team was concerned that the complexity of the rollover process, the inability to
The team was concerned that the complexity of the rollover process, the inability to
easily track resolution of identified concerns, and the lack of adequate guidance could
easily track resolution of identified concerns, and the lack of adequate guidance could
have resulted in inappropriate resolution of problems. Other examples of rollover
have resulted in inappropriate resolution of problems. Other examples of rollover
problems included: improper implementation of corrective actions, lack of cross
problems included: improper implementation of corrective actions, lack of cross
references and flawed cause analysis.
references and flawed cause analysis.
Specific examples of rollover problems identified by the team are listed below, and the
Specific examples of rollover problems identified by the team are listed below, and the
more significant ones are discussed in Sections 4OA3(2) and 4OA3(3) of this report.
more significant ones are discussed in Sections 4OA3(2) and 4OA3(3) of this report.
*       The resolution to the trisodium phosphate (TSP) post-accident concerns were
*
        difficult to evaluate due to the number of rollovers (See Section 4OA3(3)b.17 for
The resolution to the trisodium phosphate (TSP) post-accident concerns were
        details);
difficult to evaluate due to the number of rollovers (See Section 4OA3(3)b.17 for
*       Three CRs on fuel spacer grid damage were rolled into a SCAQ CR, but were
details);
        not addressed in the root cause analysis (See Section 4OA3(4)b for details);
*
*       Corrective action 13 in CR 02-05385 was not related to the identified issue.
Three CRs on fuel spacer grid damage were rolled into a SCAQ CR, but were
        Licensee determined that, due to rollovers, the corrective action ended up in the
not addressed in the root cause analysis (See Section 4OA3(4)b for details);
        wrong CR (CR 02-05385);
*
*       There were informal rollovers in CRs 02-07657, 02-05904, 02-05881, and
Corrective action 13 in CR 02-05385 was not related to the identified issue.  
        02-06779 (See Sections 4OA3(3)b.12, 4OA3(3)b.16, and 4OA3(3)b.19 for
Licensee determined that, due to rollovers, the corrective action ended up in the
        further discussions regarding rollovers); and
wrong CR (CR 02-05385);
*       In addition there was an inadequate rollover of overload protection concerns in
*
        CR 03-02616 to CR 03-03572 (Section 4OA3(2)b.2).
There were informal rollovers in CRs 02-07657, 02-05904, 02-05881, and
02-06779 (See Sections 4OA3(3)b.12, 4OA3(3)b.16, and 4OA3(3)b.19 for
further discussions regarding rollovers); and
*
In addition there was an inadequate rollover of overload protection concerns in
CR 03-02616 to CR 03-03572 (Section 4OA3(2)b.2).
The team identified that the licensee had issued seventeen CRs within a six month
The team identified that the licensee had issued seventeen CRs within a six month
period related specifically to licensee-identified concerns with the rollover process. As a
period related specifically to licensee-identified concerns with the rollover process. As a
result of the team's review of rollover CRs, the licensee identified a specific issue, as
result of the team's review of rollover CRs, the licensee identified a specific issue, as
                                          16                                      Enclosure


  documented in CR 03-01955, "CR Rollover Discrepancies," regarding rollover of
Enclosure
  concerns as part of the containment health review.
17
  Based on both the team's and the licensees own internal findings in regard to the
documented in CR 03-01955, "CR Rollover Discrepancies," regarding rollover of
  rollover process, the licensee revised the CAP procedure to place limits on the number
concerns as part of the containment health review.
  of times an issue could be rolled and to strengthen the rollover process.
Based on both the team's and the licensees own internal findings in regard to the
.3 Adequacy of Licensee's Efforts to Evaluate Identified Conditions
rollover process, the licensee revised the CAP procedure to place limits on the number
  During the inspection, the team found examples where the licensee was not fully
of times an issue could be rolled and to strengthen the rollover process.
  effective in evaluating problems, particularly in regard to determining the apparent cause
    .3
  of issues. The team determined that this failure to adequately evaluate issues could be
Adequacy of Licensee's Efforts to Evaluate Identified Conditions
  attributed to a narrow evaluation focus, weak knowledge of the design basis, and lack
During the inspection, the team found examples where the licensee was not fully
  of attention to detail.
effective in evaluating problems, particularly in regard to determining the apparent cause
  At the start of the inspection, the licensee divided CR evaluations into three categories:
of issues. The team determined that this failure to adequately evaluate issues could be
  SCAQ CRs, which required a root cause evaluation; "CA" CRs which required an
attributed to a narrow evaluation focus, weak knowledge of the design basis, and lack
  apparent cause evaluation; and "CF" CRs which required the deficiency to be fixed and
of attention to detail.
  did not require a cause evaluation.
At the start of the inspection, the licensee divided CR evaluations into three categories:
  While generally adequate, the team determined that some root cause evaluations did
SCAQ CRs, which required a root cause evaluation; "CA" CRs which required an
  not always use a formal method to arrive at a root cause. In at least one case, the root
apparent cause evaluation; and "CF" CRs which required the deficiency to be fixed and
  cause did not arrive at a cause for the discrepant condition. In another, information
did not require a cause evaluation.
  used to arrive at the conclusion was not discussed in the evaluation. In contrast, the
While generally adequate, the team determined that some root cause evaluations did
  team identified that the root cause evaluation for SCAQ CR 02-00891, performed to
not always use a formal method to arrive at a root cause. In at least one case, the root
  determine root and contributing causes of the head event, was well done.
cause did not arrive at a cause for the discrepant condition. In another, information
  In regard to the apparent causes, the team identified that the majority of the stated
used to arrive at the conclusion was not discussed in the evaluation. In contrast, the
  apparent causes were one-line sentences and appeared to address the symptoms of
team identified that the root cause evaluation for SCAQ CR 02-00891, performed to
  the deficiency and did not address why the condition happened.
determine root and contributing causes of the head event, was well done.
  The team noted that the CAP listed timeliness expectations as to when the evaluation
In regard to the apparent causes, the team identified that the majority of the stated
  (either apparent or root cause) would be completed. During the inspection, the team
apparent causes were one-line sentences and appeared to address the symptoms of
  noted that some CR evaluations were granted multiple time extensions and that other
the deficiency and did not address why the condition happened.
  evaluations were overdue by several months. The team frequently was unable to
The team noted that the CAP listed timeliness expectations as to when the evaluation
  determine the basis for the extensions being granted. Additionally, the team noted that,
(either apparent or root cause) would be completed. During the inspection, the team
  in some cases, the licensee did not have a documented basis for delaying evaluation of
noted that some CR evaluations were granted multiple time extensions and that other
  a discrepant condition until after restart. These issues were discussed with the licensee
evaluations were overdue by several months. The team frequently was unable to
  for resolution.
determine the basis for the extensions being granted. Additionally, the team noted that,
  Another concern relating to the CAP identified by the team was that the licensee's
in some cases, the licensee did not have a documented basis for delaying evaluation of
  electronic system permitted previously approved CRs to be rejected and re-evaluated.
a discrepant condition until after restart. These issues were discussed with the licensee
  The team was concerned that the process of rejecting a previously reviewed and
for resolution.
  accepted evaluation was a potential deficiency in the CAP. The licensee took corrective
Another concern relating to the CAP identified by the team was that the licensee's
  actions to discontinue this practice.
electronic system permitted previously approved CRs to be rejected and re-evaluated.  
  The team also noted that, in general, the licensee did not perform extent of condition
The team was concerned that the process of rejecting a previously reviewed and
  reviews and that the few reviews done lacked thoroughness. Revision 4 of the
accepted evaluation was a potential deficiency in the CAP. The licensee took corrective
  licensee's CAP procedure called for an assessment of generic implications on those
actions to discontinue this practice.
                                            17                                    Enclosure
The team also noted that, in general, the licensee did not perform extent of condition
reviews and that the few reviews done lacked thoroughness. Revision 4 of the
licensee's CAP procedure called for an assessment of generic implications on those


CRs requiring an apparent cause evaluation. The team noted that the lack of such
Enclosure
18
CRs requiring an apparent cause evaluation. The team noted that the lack of such
reviews created the potential for not identifying other problem areas.
reviews created the potential for not identifying other problem areas.
Specific examples of the above problems are listed below, and the more significant ones
Specific examples of the above problems are listed below, and the more significant ones
are discussed in Sections 4OA3(2) and 4OA3(3) of this report.
are discussed in Sections 4OA3(2) and 4OA3(3) of this report.
Root Cause Findings
Root Cause Findings
*       Root cause for CR 02-06178 didnt contain sufficient information to support
*
        conclusions. It also failed to address three CRs which were rolled into it.
Root cause for CR 02-06178 didnt contain sufficient information to support
        Additionally, the extent of condition review was not well documented (See
conclusions. It also failed to address three CRs which were rolled into it.  
        Section 4OA3(4)b for details);
Additionally, the extent of condition review was not well documented (See
*       Downgrade of SCAQ CRs 02-06356 and 02-06677 were not adequately justified
Section 4OA3(4)b for details);
        and, in the case of the first issue, no cause evaluation was performed at all.
*
        (See Section 4OA3(3)b.22 for details);
Downgrade of SCAQ CRs 02-06356 and 02-06677 were not adequately justified
*       Root cause was not identified for SCAQ CR 02-04673 because the finding was
and, in the case of the first issue, no cause evaluation was performed at all.  
        historical, also the evaluation failed to identify issues of pre-conditioning and
(See Section 4OA3(3)b.22 for details);
        component limitations (See Section 4OA3(3)b.15 for details);
*
Root cause was not identified for SCAQ CR 02-04673 because the finding was
historical, also the evaluation failed to identify issues of pre-conditioning and
component limitations (See Section 4OA3(3)b.15 for details);
Apparent Cause Evaluation Findings
Apparent Cause Evaluation Findings
*       Evaluation of the HPI pump minimum flow issue was inadequate (See Section
*
        4OA3(3)b.1 for details);
Evaluation of the HPI pump minimum flow issue was inadequate (See Section
*       Evaluation was inadequate in that the consequences of potentially increased
4OA3(3)b.1 for details);
        offsite doses due to the degraded condition were not addressed (See
*
        Section 4OA3(3)b.2 for details);
Evaluation was inadequate in that the consequences of potentially increased
*       Evaluation failed to address issue identified in the CR (See Section 4OA3(3)b.12
offsite doses due to the degraded condition were not addressed (See  
        for details);
Section 4OA3(3)b.2 for details);
*       Evaluation on allowable reactor coolant pump (RCP) stud elongation was flawed
*
        (See Section 4OA3(3)b.19 for details);
Evaluation failed to address issue identified in the CR (See Section 4OA3(3)b.12
*       Evaluation provided weak basis for not identifying issues (See Section
for details);
        4OA3(3)b.21 for details);
*
*       Evaluation contained incorrect information and inadequately assessed issue
Evaluation on allowable reactor coolant pump (RCP) stud elongation was flawed
        (See Section 4OA3(3)b.20 for details);
(See Section 4OA3(3)b.19 for details);
*       Evaluation of the causes for missing or degraded emergency diesel generator
*
        (EDG) tornado missile protection was poor (See Section 4OA3(3)b.23 for
Evaluation provided weak basis for not identifying issues (See Section
        details);
4OA3(3)b.21 for details);
*       Evaluation for CR 02-05640 was weak and referenced corrective action
*
        documents appeared incorrect;
Evaluation contained incorrect information and inadequately assessed issue
                                          18                                        Enclosure
(See Section 4OA3(3)b.20 for details);
*
Evaluation of the causes for missing or degraded emergency diesel generator
(EDG) tornado missile protection was poor (See Section 4OA3(3)b.23 for
details);
*
Evaluation for CR 02-05640 was weak and referenced corrective action
documents appeared incorrect;


  *       Inadequate evaluation for CR 02-05727;
Enclosure
  *       Inadequate evaluation for CR 02-05738;
19
  *       Evaluation for CR 02-05885 referenced an incorrect calculation and had a wrong
*
          revision for other another calculation;
Inadequate evaluation for CR 02-05727;
  *       Cause analysis for CR 02-06723 did not address that struts were not supposed
*
          to be greased; and
Inadequate evaluation for CR 02-05738;
  *       Evaluation did not address temperature increase for CR 02-06893
*
          (Section 4OA5(1)b.2.7).
Evaluation for CR 02-05885 referenced an incorrect calculation and had a wrong
  Extent of Condition Findings
revision for other another calculation;
  *       Extent of condition review for CR 02-00412 was inadequate (See
*
          Section 4OA3(2)b.4 for details); and
Cause analysis for CR 02-06723 did not address that struts were not supposed
  *       Required extent of condition reviews for CRs 02-01129 and 02-07188 were not
to be greased; and
          performed (See Section 4OA3(3)b.7 for details of the latter issue).
*
  At the conclusion of the inspection, the licensee initiated a collective significance review
Evaluation did not address temperature increase for CR 02-06893
  CR, 03-06908, to address the team's findings regarding CAP deficiencies, especially in
(Section 4OA5(1)b.2.7).
  the area of apparent cause evaluations.
Extent of Condition Findings
.4 Adequacy of Licensee's Efforts to Correct Identified Problems
*
  The team identified examples where inadequate corrective actions were due to the
Extent of condition review for CR 02-00412 was inadequate (See  
  inadequate cause evaluations. The team also identified examples where corrective
Section 4OA3(2)b.4 for details); and
  actions were prematurely closed based on unapproved calculations; where actions were
*
  closed without actually completing the work; and where the specified corrective actions
Required extent of condition reviews for CRs 02-01129 and 02-07188 were not
  did not resolve the originally identified issue. The team also identified several items
performed (See Section 4OA3(3)b.7 for details of the latter issue).
  where the corrective actions appeared untimely. Very few effectiveness reviews had
At the conclusion of the inspection, the licensee initiated a collective significance review
  been done at the time of the inspection, so the team was unable to assess the overall
CR, 03-06908, to address the team's findings regarding CAP deficiencies, especially in
  effectiveness of the implemented corrective actions. Most effectiveness reviews for
the area of apparent cause evaluations.
  corrective action items that were implemented via CR 02-00891 had not been completed
    .4
  by the end of the inspection.
Adequacy of Licensee's Efforts to Correct Identified Problems
  Specific examples of the above problems are listed below, and the more significant ones
The team identified examples where inadequate corrective actions were due to the
  are discussed in Sections 4OA3(2) and 4OA3(3) of this report.
inadequate cause evaluations. The team also identified examples where corrective
  *       A hardware change for CR 02-04680 was indicated as complete when it was not
actions were prematurely closed based on unapproved calculations; where actions were
          actually done;
closed without actually completing the work; and where the specified corrective actions
  *       Three examples were identified where the corrective actions were closed before
did not resolve the originally identified issue. The team also identified several items
          the calculations were issued (See Sections 4OA3(3)b.17, 4OA3(3)b.19 and
where the corrective actions appeared untimely. Very few effectiveness reviews had
          4OA5(1)b.2.23 for details);
been done at the time of the inspection, so the team was unable to assess the overall  
                                              19                                      Enclosure
effectiveness of the implemented corrective actions. Most effectiveness reviews for
corrective action items that were implemented via CR 02-00891 had not been completed
by the end of the inspection.
Specific examples of the above problems are listed below, and the more significant ones
are discussed in Sections 4OA3(2) and 4OA3(3) of this report.
*
A hardware change for CR 02-04680 was indicated as complete when it was not
actually done;
*
Three examples were identified where the corrective actions were closed before
the calculations were issued (See Sections 4OA3(3)b.17, 4OA3(3)b.19 and
4OA5(1)b.2.23 for details);


  *       The diesel driven fire pump heat load was not included in the SW ventilation
Enclosure
            system calculation, even though the NRC identified that specific heat load as one
20
            which been missed (See Section 4OA3(3)b.7 for details);
*
  *       Corrective actions to a Nuclear Quality Assurance (NQA) finding did not address
The diesel driven fire pump heat load was not included in the SW ventilation
            defined problem - NQA initiated a second CR to address the issue (Section
system calculation, even though the NRC identified that specific heat load as one
            4OA3(3)b.19);
which been missed (See Section 4OA3(3)b.7 for details);
  *       An NRC identified issue regarding a procedure deficiency was not corrected until
*
            the team questioned the issue (See Section 4OA3(3)b.12 for details);
Corrective actions to a Nuclear Quality Assurance (NQA) finding did not address
  *       Corrective action 15 to CR 02-04884 was closed even though not all required
defined problem - NQA initiated a second CR to address the issue (Section
            individuals were trained;
4OA3(3)b.19);
  *       Corrective action 30 of SCAQ CR 02-00891 was closed out prior to performing
*
            the required operations confidence reviews.
An NRC identified issue regarding a procedure deficiency was not corrected until
.5 Review of Engineering Products and Corrective Actions
the team questioned the issue (See Section 4OA3(3)b.12 for details);
  The team determined that the licensees effectiveness in resolving design deficiencies
*
  was inconsistent. The most difficult area for the licensee appeared to be in regard to
Corrective action 15 to CR 02-04884 was closed even though not all required
  quality of calculations, as many of the calculations reviewed by the team required
individuals were trained;
  multiple iterations to correct team-identified problems. The team attributed this
*
  observation to weak engineering knowledge of the design and licensing basis of the
Corrective action 30 of SCAQ CR 02-00891 was closed out prior to performing
  plant and a lack of attention to detail.
the required operations confidence reviews.
  Based on a review of recently approved mechanical engineering design calculations, the
    .5
  team determined that about 40 percent of the calculations reviewed required generation
Review of Engineering Products and Corrective Actions
  of a new CR to fix a calculation problem. Included in the problems were configuration
The team determined that the licensees effectiveness in resolving design deficiencies
  control issues where design analysis was not controlled. The team also noted use of
was inconsistent. The most difficult area for the licensee appeared to be in regard to
  non-conservative assumptions, omissions, and errors in recently approved design
quality of calculations, as many of the calculations reviewed by the team required
  calculations.
multiple iterations to correct team-identified problems. The team attributed this
  In the electrical area, the team determined that the electric transient analysis profile
observation to weak engineering knowledge of the design and licensing basis of the
  (ETAP) calculations which were completed in 2003, appeared to be well performed.
plant and a lack of attention to detail.
  As a result of the numerous calculational issues identified by the team, the licensee
Based on a review of recently approved mechanical engineering design calculations, the
  initiated CR 03-06907 to perform a collective significance review on calculation quality.
team determined that about 40 percent of the calculations reviewed required generation
  Additionally, the licensee initiated CR 03-06909 to perform a collective significance
of a new CR to fix a calculation problem. Included in the problems were configuration
  review of overall engineering design control issues.
control issues where design analysis was not controlled. The team also noted use of
  Subsequent to the onsite inspection, on November 12 and December 10, 2003, the
non-conservative assumptions, omissions, and errors in recently approved design
  licensee presented to the NRC, the planned actions to address the issues and concerns
calculations.
  identified by the CATI. As part of these meetings, the licensee made a number of
In the electrical area, the team determined that the electric transient analysis profile
  commitments to further improve the quality of engineering products such as calculations
(ETAP) calculations which were completed in 2003, appeared to be well performed.
  and cause analyses. These efforts included expanding the scope of the Engineering
As a result of the numerous calculational issues identified by the team, the licensee
  Assessment Board (EAB) reviews to include calculations which supported modifications.
initiated CR 03-06907 to perform a collective significance review on calculation quality.  
  The process improvements were incorporated as part of the licensees Operational
Additionally, the licensee initiated CR 03-06909 to perform a collective significance
  Improvement Plan for Cycle 14, Revision 3.
review of overall engineering design control issues.
                                            20                                      Enclosure
Subsequent to the onsite inspection, on November 12 and December 10, 2003, the
licensee presented to the NRC, the planned actions to address the issues and concerns
identified by the CATI. As part of these meetings, the licensee made a number of
commitments to further improve the quality of engineering products such as calculations
and cause analyses. These efforts included expanding the scope of the Engineering
Assessment Board (EAB) reviews to include calculations which supported modifications.  
The process improvements were incorporated as part of the licensees Operational
Improvement Plan for Cycle 14, Revision 3.


  .6 Adequacy of Licensees Efforts to Resolve Procedure Adherence and Quality
Enclosure
      Issues
21
      The team noted that there were several programmatic procedural improvements,
    .6
      including the CAP procedure, the boric acid corrosion control (BACC) program
Adequacy of Licensees Efforts to Resolve Procedure Adherence and Quality
      procedure, and the self-assessment guideline. Additionally, engineering procedures
Issues
      also improved. Typically, it appeared that the licensee staff did a good job on procedure
The team noted that there were several programmatic procedural improvements,
      development. The team also noted that the licensee identified a number of procedural
including the CAP procedure, the boric acid corrosion control (BACC) program
      adherence problems. The licensee initiated a SCAQ CR in 2002 to evaluate and
procedure, and the self-assessment guideline. Additionally, engineering procedures
      address multiple procedure issues.
also improved. Typically, it appeared that the licensee staff did a good job on procedure
      Many of the teams findings resulted from the licensees failure to adhere to the
development. The team also noted that the licensee identified a number of procedural
      corrective action procedure and other procedural requirements. Specific examples of
adherence problems. The licensee initiated a SCAQ CR in 2002 to evaluate and
      the above problems are listed below, and the more significant ones are discussed in
address multiple procedure issues.
      Sections 4OA3(2) and 4OA3(3) of this report.
Many of the teams findings resulted from the licensees failure to adhere to the
      *       The licensee failed to follow trending and self evaluation procedures and
corrective action procedure and other procedural requirements. Specific examples of
              guidelines (See Section 4OA2(2)b.1).
the above problems are listed below, and the more significant ones are discussed in
      *       The licensee's NQA organization identified numerous problems with procedures
Sections 4OA3(2) and 4OA3(3) of this report.
              (See Section 4OA2(2)b.3 for detail).
*
(2)   Review of the Licensees Internal Assessment Activities
The licensee failed to follow trending and self evaluation procedures and
a.   Inspection Scope
guidelines (See Section 4OA2(2)b.1).
      The team examined the licensees program, and implementation thereof, to trend CRs
*
      and analyze the results as delineated in procedures NG-NA-00711, NOBP-LP-2001 and
The licensee's NQA organization identified numerous problems with procedures
      NOBP-LP-2004. In addition, the team examined the licensees implementation of the
(See Section 4OA2(2)b.3 for detail).
      self assessment program. Trending and self assessments were required by the
(2)
      licensee's procedures. The team also reviewed the licensees implementation of CAP
Review of the Licensees Internal Assessment Activities
      performance indicators (PIs) to determine their intended use and adequacy in
  a.
      measuring effectiveness of corrective action implementation. The team also evaluated
Inspection Scope
      the effectiveness of the licensee's internal assessment capability by reviewing selected
The team examined the licensees program, and implementation thereof, to trend CRs
      NQA audits and available self evaluation reports, which were specifically performed to
and analyze the results as delineated in procedures NG-NA-00711, NOBP-LP-2001 and
      assess the implementation of the CAP and which were conducted between January
NOBP-LP-2004. In addition, the team examined the licensees implementation of the
      2002 and August 2003. In addition, the team reviewed the licensees follow-up on
self assessment program. Trending and self assessments were required by the
      selected NQA findings to determine whether the licensees response was adequate and
licensee's procedures. The team also reviewed the licensees implementation of CAP
      timely, and corrective actions were properly prioritized and implemented to prevent
performance indicators (PIs) to determine their intended use and adequacy in
      recurrence. The procedure for audit activities performed by the NQA organization was
measuring effectiveness of corrective action implementation. The team also evaluated
      described in procedure NOP-LP-2004.
the effectiveness of the licensee's internal assessment capability by reviewing selected
b.   Observations and Findings
NQA audits and available self evaluation reports, which were specifically performed to
  .1 Trending, Self-Assessment, and Evaluation Program Implementation
assess the implementation of the CAP and which were conducted between January
      Introduction: The team identified that the licensee failed to perform the required CR
2002 and August 2003. In addition, the team reviewed the licensees follow-up on
      trending analysis and to ensure that condition reports were regularly assessed for
selected NQA findings to determine whether the licensees response was adequate and
      indications of adverse trends, generic problems, and repetitive conditions requiring
timely, and corrective actions were properly prioritized and implemented to prevent
                                                21                                    Enclosure
recurrence. The procedure for audit activities performed by the NQA organization was
described in procedure NOP-LP-2004.
  b.
Observations and Findings
    .1
Trending, Self-Assessment, and Evaluation Program Implementation
Introduction: The team identified that the licensee failed to perform the required CR
trending analysis and to ensure that condition reports were regularly assessed for
indications of adverse trends, generic problems, and repetitive conditions requiring


corrective actions. The licensee entered the issue into its corrective action program in
Enclosure
22
corrective actions. The licensee entered the issue into its corrective action program in
December 2002 and again in July 2003 to re-evaluate the issue, and began the required
December 2002 and again in July 2003 to re-evaluate the issue, and began the required
trending at the end of the inspection.
trending at the end of the inspection.
Description: The team determined, through reviews of CRs and via interviews that the
Description: The team determined, through reviews of CRs and via interviews that the
licensee had not implemented the CR trending program which was required by
licensee had not implemented the CR trending program which was required by
procedure NG-NA-00711. In April 2003, the team determined that trending of
procedure NG-NA-00711. In April 2003, the team determined that trending of
equipment CRs stopped in December 2001, prior to the plant shutting down for refueling
equipment CRs stopped in December 2001, prior to the plant shutting down for refueling
outage (RFO). Departmental and performance improvement group trending activities
outage (RFO). Departmental and performance improvement group trending activities
stopped in March 2002. This latter cessation was a licensee management decision
stopped in March 2002. This latter cessation was a licensee management decision
because of the number of issues which were being identified during the various
because of the number of issues which were being identified during the various
programmatic reviews. However, once the programmatic reviews were completed, the
programmatic reviews. However, once the programmatic reviews were completed, the
trending program was not reinitiated in a timely fashion.
trending program was not reinitiated in a timely fashion.
Procedure NG-NA-00711 required that CR trending analysis be performed regularly.
Procedure NG-NA-00711 required that CR trending analysis be performed regularly.  
Section 6.2 of the procedure stated that the performance improvement manager was to
Section 6.2 of the procedure stated that the performance improvement manager was to
ensure that CRs were regularly assessed for indications of adverse trends, generic
ensure that CRs were regularly assessed for indications of adverse trends, generic
problems, and repetitive conditions requiring corrective actions. The procedure also
problems, and repetitive conditions requiring corrective actions. The procedure also
required that indications of potential adverse conditions were to be discussed with
required that indications of potential adverse conditions were to be discussed with
management of the responsible organization to ensure that generic problems, repetitive
management of the responsible organization to ensure that generic problems, repetitive
conditions or adverse trends were classified as conditions adverse to quality. In
conditions or adverse trends were classified as conditions adverse to quality. In
addition, the procedure stated that a quality trend summary was to be prepared at least
addition, the procedure stated that a quality trend summary was to be prepared at least
quarterly and distributed to managers, directors and the Vice President - Nuclear.
quarterly and distributed to managers, directors and the Vice President - Nuclear.
The team determined that a licensee engineer initiated CR 02-10369 on
The team determined that a licensee engineer initiated CR 02-10369 on
December 19, 2002, to document that the CR trend analysis had not been reinitiated
December 19, 2002, to document that the CR trend analysis had not been reinitiated
even though the discovery phase of the various programmatic reviews was finished.
even though the discovery phase of the various programmatic reviews was finished.  
The CR identified that procedural requirements for trend analysis were not being
The CR identified that procedural requirements for trend analysis were not being
followed. The CR also stated that a regular review of CR issues was also required as a
followed. The CR also stated that a regular review of CR issues was also required as a
corrective action to a previous audit finding. The licensees evaluation of CR 02-10369
corrective action to a previous audit finding. The licensees evaluation of CR 02-10369
noted that, although the procedurally required trend analysis and trend reporting had not
noted that, although the procedurally required trend analysis and trend reporting had not
been resumed, other tasks enacted under the Davis-Besse return to service plan could
been resumed, other tasks enacted under the Davis-Besse return to service plan could
have identified generic problems, adverse trends and repetitive conditions. Therefore,
have identified generic problems, adverse trends and repetitive conditions. Therefore,
the licensee concluded that no immediate corrective actions were necessary to reinstate
the licensee concluded that no immediate corrective actions were necessary to reinstate
the CR trending program.
the CR trending program.
The team noted that trend analysis and reporting should contribute to the identification
The team noted that trend analysis and reporting should contribute to the identification
of potential adverse trends, repetitive conditions, and generic problems before those
of potential adverse trends, repetitive conditions, and generic problems before those
trends become significant issues. Programmatic issues were identified by the team
trends become significant issues. Programmatic issues were identified by the team
during the inspection, such as inappropriate use of rollovers, calculation problems and
during the inspection, such as inappropriate use of rollovers, calculation problems and
design issues. The team noted that the licensee initiated three condition reports to
design issues. The team noted that the licensee initiated three condition reports to
evaluate the collective significance of the team's findings.
evaluate the collective significance of the team's findings.  
On July 23, 2003, NQA independently initiated CR 03-05925 which documented
On July 23, 2003, NQA independently initiated CR 03-05925 which documented
concerns identical to the team's concerns in regard to weaknesses in implementation of
concerns identical to the team's concerns in regard to weaknesses in implementation of
trending and non-compliance with trending requirements. NQA identified that, in most
trending and non-compliance with trending requirements. NQA identified that, in most
organizations, activity codes and trend codes were not routinely trended or analyzed and
organizations, activity codes and trend codes were not routinely trended or analyzed and
that management involvement with trending, in some organizations, was minimal or
that management involvement with trending, in some organizations, was minimal or
nonexistent.
nonexistent.
                                          22                                    Enclosure


  The team determined that the framework for an effective trending program existed, but it
Enclosure
  was not being implemented and that management attention and focus was needed in
23
  order to ensure that the programs were reinstated. Due to the team identifying potential
The team determined that the framework for an effective trending program existed, but it
  trends in several areas, the team was unable to confirm the licensees position that
was not being implemented and that management attention and focus was needed in
  reliance on processes developed for the extended shutdown could substitute for the
order to ensure that the programs were reinstated. Due to the team identifying potential
  trending analysis process. The licensee entered the issue into its corrective action
trends in several areas, the team was unable to confirm the licensees position that
  program in December 2002 and again in July 2003 to re-assess the issue, and re-
reliance on processes developed for the extended shutdown could substitute for the
  instituted the required trending at the end of the inspection.
trending analysis process. The licensee entered the issue into its corrective action
  The team also assessed the licensees self assessment program implementation. The
program in December 2002 and again in July 2003 to re-assess the issue, and re-
  need for a self assessment and evaluation program was delineated in NOBP-LP-2001,
instituted the required trending at the end of the inspection.
  NOBP-LP-2004, and the Davis-Besse self evaluation process guide. The purpose of
The team also assessed the licensees self assessment program implementation. The
  these self assessment and evaluation guidelines was to continue plant improvement
need for a self assessment and evaluation program was delineated in NOBP-LP-2001,
  through implementation of learning organization behaviors by the Davis-Besse
NOBP-LP-2004, and the Davis-Besse self evaluation process guide. The purpose of
  management team to periodically critically assess organizational performance against
these self assessment and evaluation guidelines was to continue plant improvement
  established standards/expectations of performance and industry-best practices. The
through implementation of learning organization behaviors by the Davis-Besse
  self evaluation was intended to identify organizational strengths, weaknesses,
management team to periodically critically assess organizational performance against
  challenges, and areas of improvements.
established standards/expectations of performance and industry-best practices. The
  The self evaluation process guideline stated that each quarter, the section managers
self evaluation was intended to identify organizational strengths, weaknesses,
  and directors were to present the results from their self-evaluations to the Davis-Besse
challenges, and areas of improvements.
  Vice President. In April 2003, the team noted that the licensee stopped performing the
The self evaluation process guideline stated that each quarter, the section managers
  required self evaluations by the different plant departments after the first quarter in
and directors were to present the results from their self-evaluations to the Davis-Besse
  2002. In July 2003, NQA identified in CR 03-05925 that most site organizations were
Vice President. In April 2003, the team noted that the licensee stopped performing the
  not actively performing self-evaluations. The licensee was in the process of replacing
required self evaluations by the different plant departments after the first quarter in
  the guideline and reinstating the self-evaluations at the end of the inspection.
2002. In July 2003, NQA identified in CR 03-05925 that most site organizations were
  Analysis: The team determined that a performance deficiency existed because the
not actively performing self-evaluations. The licensee was in the process of replacing
  licensee failed to perform the required CR trending. Since there was a performance
the guideline and reinstating the self-evaluations at the end of the inspection.
  deficiency, the team compared this performance deficiency to the minor questions
Analysis: The team determined that a performance deficiency existed because the
  contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
licensee failed to perform the required CR trending. Since there was a performance
  Reports." The team concluded that the issue was minor because the lack of CR
deficiency, the team compared this performance deficiency to the minor questions
  trending occurred while the unit was shutdown.
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
  Enforcement: The failure to perform CR trending and department self evaluations from
Reports." The team concluded that the issue was minor because the lack of CR
  March 2002 until the end of the CATI on-site inspection in September 2003, constitutes
trending occurred while the unit was shutdown.  
  a violation of 10 CFR Appendix B, Criterion V, which has minor significance and is not
Enforcement: The failure to perform CR trending and department self evaluations from
  subject to enforcement action in accordance with Section IV of the NRCs Enforcement
March 2002 until the end of the CATI on-site inspection in September 2003, constitutes
  Policy.
a violation of 10 CFR Appendix B, Criterion V, which has minor significance and is not
  While minor violations are not normally documented in inspection reports, the team
subject to enforcement action in accordance with Section IV of the NRCs Enforcement
  determined that documentation was appropriate in this case based on the length of time
Policy.
  the licensee was not in compliance.
While minor violations are not normally documented in inspection reports, the team
.2 Corrective Action Program Performance Indicators
determined that documentation was appropriate in this case based on the length of time
  During the period when the licensee was not performing trending or self-evaluations, PIs
the licensee was not in compliance.
  on the restart performance and CAP effectiveness were published weekly. The CAP
    .2
  effectiveness PIs included corrective action effectiveness, CR category accuracy, CR
Corrective Action Program Performance Indicators
  evaluations, corrective action resolution, CR self identification, and management
During the period when the licensee was not performing trending or self-evaluations, PIs
                                            23                                      Enclosure
on the restart performance and CAP effectiveness were published weekly. The CAP
effectiveness PIs included corrective action effectiveness, CR category accuracy, CR
evaluations, corrective action resolution, CR self identification, and management


  observations. Restart PIs relating to CAP implementation included CR evaluations, CR
Enclosure
  resolution, root cause evaluation quality, program and process error rate, CR category
24
  accuracy, CR operations review, corrective action resolution and CR self-identified rate.
observations. Restart PIs relating to CAP implementation included CR evaluations, CR
  The team noted that the indicators generally showed improving trends and that, in most
resolution, root cause evaluation quality, program and process error rate, CR category
  cases, the licensee was meeting established goals. Action plans were in place for those
accuracy, CR operations review, corrective action resolution and CR self-identified rate.
  PIs which were not meeting their goal in order to improve performance prior to restart.
The team noted that the indicators generally showed improving trends and that, in most
  The team reviewed these PIs and determined that the PIs generally reflected CAP
cases, the licensee was meeting established goals. Action plans were in place for those
  performance. The team noted that, for example, PI P-01, "Corrective Action Program
PIs which were not meeting their goal in order to improve performance prior to restart.
  Implementation," rated CAP implementation from January to September 2003 as Red
The team reviewed these PIs and determined that the PIs generally reflected CAP
  for six of the nine months and as Yellow for the remaining three months. During the
performance. The team noted that, for example, PI P-01, "Corrective Action Program
  review of P-01, the team noted that the licensee has routinely determined that the
Implementation," rated CAP implementation from January to September 2003 as Red
  "Repeat Events" element was Green. This meant that there were no repeat SCAQ
for six of the nine months and as Yellow for the remaining three months. During the
  events in the last two years. The team determined that, in 2002, the licensee initiated
review of P-01, the team noted that the licensee has routinely determined that the
  six SCAQ CRs for what appeared to be a recurring trend of untimely and ineffective
"Repeat Events" element was Green. This meant that there were no repeat SCAQ
  CAP resolution and program implementation. These included CRs 02-02419, 02-02584,
events in the last two years. The team determined that, in 2002, the licensee initiated
  02-03497, 02-03674, 02-04884 and 02-07328. The licensee stated that the above
six SCAQ CRs for what appeared to be a recurring trend of untimely and ineffective
  SCAQ CRs could not be considered repeat events because the events did not involve
CAP resolution and program implementation. These included CRs 02-02419, 02-02584,
  similar tasks, causes and consequences. Based on the licensees definition, SCAQ
02-03497, 02-03674, 02-04884 and 02-07328. The licensee stated that the above
  CRs had to be identical in all three (tasks, causes and consequences) as well as
SCAQ CRs could not be considered repeat events because the events did not involve
  occurring within two years of each other in order for them to be considered as a repeat
similar tasks, causes and consequences. Based on the licensees definition, SCAQ
  event. The team considered the licensees definition to be limiting, as the above CRs
CRs had to be identical in all three (tasks, causes and consequences) as well as
  appeared to the team to document repeat events and an adverse trends. The team also
occurring within two years of each other in order for them to be considered as a repeat
  noted that, because the licensee limited the definition of repeat events to SCAQ CRs,
event. The team considered the licensees definition to be limiting, as the above CRs
  low level issues that were occurring on a repeat basis (such as repeat CRs) did not
appeared to the team to document repeat events and an adverse trends. The team also
  show up in the PI.
noted that, because the licensee limited the definition of repeat events to SCAQ CRs,
  The team noted that the PIs did not always provide an accurate indication of the health
low level issues that were occurring on a repeat basis (such as repeat CRs) did not
  of the CAP implementation. For example, the team identified a number of examples
show up in the PI.
  where CRs were indicated as closed in the system when, in reality, the issues were
The team noted that the PIs did not always provide an accurate indication of the health
  transferred to other CRs and may not have been either evaluated or corrected.
of the CAP implementation. For example, the team identified a number of examples
  Finally, the team noted that the PI which assessed quality of engineering products had
where CRs were indicated as closed in the system when, in reality, the issues were
  shown a negative trend for five weeks from the end of July to the beginning of August
transferred to other CRs and may not have been either evaluated or corrected.
  2003. Despite the negative trend, the indicator stated that engineering product quality
Finally, the team noted that the PI which assessed quality of engineering products had
  had significantly improved since initiation of the EAB. The team questioned the licensee
shown a negative trend for five weeks from the end of July to the beginning of August
  as to the positive statement on the trend report when the graph had been showing a
2003. Despite the negative trend, the indicator stated that engineering product quality
  declining trend in quality of engineering products. After questioning by the team, the
had significantly improved since initiation of the EAB. The team questioned the licensee
  licensee examined additional engineering products and informed the team that the
as to the positive statement on the trend report when the graph had been showing a
  products had improved and the latest trend information reflected that improvement.
declining trend in quality of engineering products. After questioning by the team, the
.3 Nuclear Quality Assessment Audits and Self Assessments of Corrective Action
licensee examined additional engineering products and informed the team that the
  Program Implementation
products had improved and the latest trend information reflected that improvement.
  The NQA organization conducted various performance-based and program-based
    .3
  audits of the CAP and its implementation. Some audits evaluated specific activities,
Nuclear Quality Assessment Audits and Self Assessments of Corrective Action
  while other audits were broad evaluations of processes or department performance.
Program Implementation
  Generally, the team found NQA audits to be of a critical nature and to adequately
The NQA organization conducted various performance-based and program-based
                                            24                                    Enclosure
audits of the CAP and its implementation. Some audits evaluated specific activities,
while other audits were broad evaluations of processes or department performance.  
Generally, the team found NQA audits to be of a critical nature and to adequately


    identify CAP implementation deficiencies. The NQA auditors identified conditions
Enclosure
    adverse to quality which were documented on CRs and tracked in the CR database.
25
    NQA used the following performance categories to rate effectiveness of the
identify CAP implementation deficiencies. The NQA auditors identified conditions
    implementation of CAP: Good Performance, Satisfactory Performance, Marginal
adverse to quality which were documented on CRs and tracked in the CR database.
    Performance and Unacceptable Performance. The table below documents the results
NQA used the following performance categories to rate effectiveness of the
    of the six NQA audits reviewed by the team:
implementation of CAP: Good Performance, Satisfactory Performance, Marginal
    NQA Rating of Corrective Action Program Implementation
Performance and Unacceptable Performance. The table below documents the results
    Report Number           Date Completed         Primary Rating         Elements Rating
of the six NQA audits reviewed by the team:
    DB-C-02-02               August 9, 2002         Marginal               Unacceptable
NQA Rating of Corrective Action Program Implementation
    DB-C-02-03               November 14, 2002     Marginal               Unacceptable
Report Number
    DB-C-02-04               February 19, 2003     Not Rated             Marginal
Date Completed
    DB-C-03-01               May 28, 2003           Not Rated             Marginal
Primary Rating
    DB-C-03-02               September 1, 2003     Satisfactory1         Not Rated
Elements Rating
    DB-C-03-03               November 17, 2003     Marginal               Not Rated
DB-C-02-02
    1
August 9, 2002
      Note: The "satisfactory" rating was for the overall CAP and did not focus on
Marginal
    implementation.
Unacceptable
    The team noted that the selected CAP implementation areas assessed by NQA from
DB-C-02-03
    March 2002 to October 2003 were rated as either "marginal" or "unacceptable." For
November 14, 2002
    example, a NQA CAP focused assessment was conducted between April 4 through
Marginal
    July 4, 2003, and identified CAP and implementation deficiencies which were similar to
Unacceptable
    those identified by the NRC CATI (NQA initiated 24 CRs). Examples included: lack of
DB-C-02-04
    trending activities to identify adverse to quality conditions, use of PI to assess CAP, less
February 19, 2003
    than adequate cause evaluations, corrective action item implementation timeliness, poor
Not Rated
    documentation of corrective actions, inadequate peer reviews, lack of rigor,
Marginal
    configuration control issues, rollovers concerns, and failure to comply with administrative
DB-C-03-01
    requirements of the NOP (mostly by engineering). Similar findings were noted during
May 28, 2003
    the November 2003 NQA audit.
Not Rated
    Overall, the team concluded that NQA was performing sufficiently probing assessments
Marginal
    of the licensees corrective action program implementation.
DB-C-03-02
(3) Management CAP Meetings
September 1, 2003
a. Inspection Scope
Satisfactory1
    One of the key building blocks in the licensees return to service plan was the
Not Rated
    management and human performance excellence plan. The purpose of this plan was to
DB-C-03-03
    address the fact that, "management ineffectively implemented processes, and thus
November 17, 2003
                                              25                                      Enclosure
Marginal
Not Rated
1Note: The "satisfactory" rating was for the overall CAP and did not focus on
implementation.
The team noted that the selected CAP implementation areas assessed by NQA from
March 2002 to October 2003 were rated as either "marginal" or "unacceptable." For
example, a NQA CAP focused assessment was conducted between April 4 through
July 4, 2003, and identified CAP and implementation deficiencies which were similar to
those identified by the NRC CATI (NQA initiated 24 CRs). Examples included: lack of
trending activities to identify adverse to quality conditions, use of PI to assess CAP, less
than adequate cause evaluations, corrective action item implementation timeliness, poor
documentation of corrective actions, inadequate peer reviews, lack of rigor,
configuration control issues, rollovers concerns, and failure to comply with administrative
requirements of the NOP (mostly by engineering). Similar findings were noted during
the November 2003 NQA audit.
Overall, the team concluded that NQA was performing sufficiently probing assessments
of the licensees corrective action program implementation.
(3)
Management CAP Meetings
  a.
Inspection Scope
One of the key building blocks in the licensees return to service plan was the
management and human performance excellence plan. The purpose of this plan was to
address the fact that, "management ineffectively implemented processes, and thus


  failed to detect and address plant problems as opportunities arose." One of the primary
Enclosure
  management contributors to this failure was the ineffective implementation of the CAP.
26
  During this inspection, the team attended and assessed the licensee management
failed to detect and address plant problems as opportunities arose." One of the primary
  activities and involvement in selected corrective action related meetings. During these
management contributors to this failure was the ineffective implementation of the CAP.
  meetings the licensee conducted a review and classification of CRs, evaluated and
During this inspection, the team attended and assessed the licensee management
  performed a critique of root cause and engineering products, prioritized work activities,
activities and involvement in selected corrective action related meetings. During these
  and provided work completion schedule extensions for ongoing work activities. The
meetings the licensee conducted a review and classification of CRs, evaluated and
  team attended and observed various corrective action management oversite meetings
performed a critique of root cause and engineering products, prioritized work activities,
  including the corrective action review board (CARB), the restart station review board
and provided work completion schedule extensions for ongoing work activities. The
  (RSRB), and the management review board (MRB).
team attended and observed various corrective action management oversite meetings
b. Observations and Findings
including the corrective action review board (CARB), the restart station review board
  Corrective Action Review Board Meetings: The purpose of the meetings was to
(RSRB), and the management review board (MRB).
  evaluate completed root causes performed to identify and address causes of more
  b.
  significant plant related issues which were documented in CRs. The team concluded
Observations and Findings
  that the CARB was comprised of experienced individuals with a wide range of
Corrective Action Review Board Meetings: The purpose of the meetings was to
  knowledge. The CARB was primarily involved in reviewing the cause analysis packages
evaluate completed root causes performed to identify and address causes of more
  for completeness and adequacy of technical information. The CARB also concentrated
significant plant related issues which were documented in CRs. The team concluded
  on potential design and safety issues and ensured that the engineering
that the CARB was comprised of experienced individuals with a wide range of
  recommendations for resolution of the identified issues appeared adequate to address
knowledge. The CARB was primarily involved in reviewing the cause analysis packages
  the causes.
for completeness and adequacy of technical information. The CARB also concentrated
  Restart Station Review Board: One of the purposes of the RSRB was to screen and
on potential design and safety issues and ensured that the engineering
  classify CRs as to whether they needed to be addressed prior to restart. The team
recommendations for resolution of the identified issues appeared adequate to address
  noted that CRs were screened and classified into one of four categories based on
the causes.
  whether the corrective actions: (1) were necessary to address NRC Manual Chapter
Restart Station Review Board: One of the purposes of the RSRB was to screen and
  (MC) 0350, "Oversight of Operating Reactor Facilities in an Extended Shutdown as a
classify CRs as to whether they needed to be addressed prior to restart. The team
  Result of Significant Performance Problems" issues; (2) were necessary to address
noted that CRs were screened and classified into one of four categories based on
  Davis-Besse restart expectations; (3) could be implemented following plant restart; or
whether the corrective actions: (1) were necessary to address NRC Manual Chapter
  (4) could be addressed at a time unrelated to plant restart. Once the licensee staff
(MC) 0350, "Oversight of Operating Reactor Facilities in an Extended Shutdown as a
  developed corrective actions to address the issues documented in the CRs, the RSRB
Result of Significant Performance Problems" issues; (2) were necessary to address
  also screened the proposed corrective actions to ensure that the underlying issues were
Davis-Besse restart expectations; (3) could be implemented following plant restart; or
  fully addressed. The team observed RSRB members interactions and noted good
(4) could be addressed at a time unrelated to plant restart. Once the licensee staff
  questioning attitude and generally appropriate classification of CRs.
developed corrective actions to address the issues documented in the CRs, the RSRB
  Management Review Board: During the MRB meetings, the licensee discussed
also screened the proposed corrective actions to ensure that the underlying issues were
  corrective action items including review of latest initiated CRs and the potential for
fully addressed. The team observed RSRB members interactions and noted good
  indications of adverse trends. Management appeared to be engaged in the CAP during
questioning attitude and generally appropriate classification of CRs.
  these meetings.
Management Review Board: During the MRB meetings, the licensee discussed
  Three Day Look-Ahead Committee: This committee discussed CR status and due
corrective action items including review of latest initiated CRs and the potential for
  dates. The team attended several meetings at the beginning of the inspection and
indications of adverse trends. Management appeared to be engaged in the CAP during
  noted that many due dates were being extended without formal justification or
these meetings.
  documented management approval. After the team commented on this practice, the
Three Day Look-Ahead Committee: This committee discussed CR status and due
  licensee no longer allowed informal extensions.
dates. The team attended several meetings at the beginning of the inspection and
                                          26                                        Enclosure
noted that many due dates were being extended without formal justification or
documented management approval. After the team commented on this practice, the
licensee no longer allowed informal extensions.  


    The team concluded that the management meetings and processes had an appropriate
Enclosure
    approach for evaluating and characterizing newly identified issues. The members
27
    appeared to be qualified and knowledgeable of the requirements.
The team concluded that the management meetings and processes had an appropriate
approach for evaluating and characterizing newly identified issues. The members
appeared to be qualified and knowledgeable of the requirements.
4OA3 Event Response Follow-up - Special Inspection (71153 and 93812)
4OA3 Event Response Follow-up - Special Inspection (71153 and 93812)
(1) Background
(1)
    Davis-Besse CAP Compliance Review
Background
    As part of the licensees restart action plan to identify, monitor and complete all actions
Davis-Besse CAP Compliance Review
    necessary for safe and reliable return to service the licensee initiated various teams
As part of the licensees restart action plan to identify, monitor and complete all actions
    which were tasked with reviewing selected plant programs to ensure that the programs
necessary for safe and reliable return to service the licensee initiated various teams
    were fulfilling required obligations and were acceptable to support plant restart. The
which were tasked with reviewing selected plant programs to ensure that the programs
    CAP was selected as one of the plant programs to receive a comprehensive Phase 2
were fulfilling required obligations and were acceptable to support plant restart. The
    review as described in the Davis-Besse program compliance plan and procedure
CAP was selected as one of the plant programs to receive a comprehensive Phase 2
    NG-EN-00385.
review as described in the Davis-Besse program compliance plan and procedure
    The review was conducted between June 10 and August 9, 2002. Results were
NG-EN-00385.
    documented in the "Corrective Action Program Review" report and included numerous
The review was conducted between June 10 and August 9, 2002. Results were
    concerns relative to the CAP process and implementation. The Phase 2 review team
documented in the "Corrective Action Program Review" report and included numerous
    determined that the CAP generally met regulatory requirements and that the identified
concerns relative to the CAP process and implementation. The Phase 2 review team
    problems were primarily associated with program implementation. However, the review
determined that the CAP generally met regulatory requirements and that the identified
    team also concluded that the CAP was not consistently implemented in full compliance
problems were primarily associated with program implementation. However, the review
    with the spirit and letter of the governing and implementing documents and that the CAP
team also concluded that the CAP was not consistently implemented in full compliance
    needed to be strengthened prior to restart of the plant.
with the spirit and letter of the governing and implementing documents and that the CAP
    The primary problem identified during this review was summarized as, "inadequate
needed to be strengthened prior to restart of the plant.
    implementation of the CAP." Examples of ineffective CAP implementation issues
The primary problem identified during this review was summarized as, "inadequate
    identified as a result of this review included: (1) a reluctance to identify conditions
implementation of the CAP." Examples of ineffective CAP implementation issues
    adverse to quality relating to organizational, human performance and programs in a CR;
identified as a result of this review included: (1) a reluctance to identify conditions
    (2) a recurring trend of inadequate CR cause evaluations and corrective actions; (3) a
adverse to quality relating to organizational, human performance and programs in a CR;
    recurring trend of inadequate, untimely, ineffective and improperly closed corrective
(2) a recurring trend of inadequate CR cause evaluations and corrective actions; (3) a
    actions; (4) MRB deficiencies; (5) a need for improvement in the trending program; (6)
recurring trend of inadequate, untimely, ineffective and improperly closed corrective
    untimely resolution of issues and supervisory and senior reactor operator reviews; (7)
actions; (4) MRB deficiencies; (5) a need for improvement in the trending program; (6)
    ineffective corrective action to preclude repetition; and (8) recurring trend of procedure
untimely resolution of issues and supervisory and senior reactor operator reviews; (7)
    non-compliance. These and other findings were determined to be consistent with the
ineffective corrective action to preclude repetition; and (8) recurring trend of procedure
    root cause analysis reports for CR 02-00891.
non-compliance. These and other findings were determined to be consistent with the
    To resolve the identified deficiencies and to improve program implementation, the
root cause analysis reports for CR 02-00891.
    licensee generated numerous CRs that included recommended corrective actions to
To resolve the identified deficiencies and to improve program implementation, the
    resolve and correct the noted deficiencies. The majority of the CRs from the review
licensee generated numerous CRs that included recommended corrective actions to
    were classified as requiring evaluation and resolution prior to restart, although some
resolve and correct the noted deficiencies. The majority of the CRs from the review
    were classified as post restart. Many of the corrective action items were rolled into
were classified as requiring evaluation and resolution prior to restart, although some
    CR 02-04884. As part of the corrective actions to address these findings the licensee
were classified as post restart. Many of the corrective action items were rolled into
    determined that training of staff and changes to the program documents were necessary
CR 02-04884. As part of the corrective actions to address these findings the licensee
    in order to restore an effective CAP.
determined that training of staff and changes to the program documents were necessary
                                                27                                      Enclosure
in order to restore an effective CAP.


      Assessment of the Corrective Action Program Compliance Review
Enclosure
      The CATI team reviewed selected corrective actions to determine the effectiveness of
28
      the licensees implementation of the specified corrective actions. The team determined
Assessment of the Corrective Action Program Compliance Review
      the licensees Phase 2 review of the CAP was comprehensive and in accordance with
The CATI team reviewed selected corrective actions to determine the effectiveness of
      procedure NG-EN-00385. The team concluded that the CAP appeared to contain many
the licensees implementation of the specified corrective actions. The team determined
      of the programmatic elements needed for a successful program; however, station
the licensees Phase 2 review of the CAP was comprehensive and in accordance with
      personnel did not consistently identify or effectively resolve plant issues. This was
procedure NG-EN-00385. The team concluded that the CAP appeared to contain many
      demonstrated by the team identifying many of the same issues as those identified in the
of the programmatic elements needed for a successful program; however, station
      Phase 2 review.
personnel did not consistently identify or effectively resolve plant issues. This was
(2)   Detailed Team Review of Licensee Corrective Actions Implemented to Address
demonstrated by the team identifying many of the same issues as those identified in the
      Electrical Issues Previously Identified by NRC or the Licensee
Phase 2 review.
a.   Inspection Scope
(2)
      The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,
Detailed Team Review of Licensee Corrective Actions Implemented to Address
      and resolve the identified equipment, human performance and/or programmatic adverse
Electrical Issues Previously Identified by NRC or the Licensee
      to quality plant conditions. The team mainly focused on plant systems design and
  a.
      licensing basis requirements issues which were previously identified by the NRC, the
Inspection Scope
      licensee and others during various design reviews conducted in 2002. The team
The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,
      assessed effectiveness of the licensees corrective actions implemented to address
and resolve the identified equipment, human performance and/or programmatic adverse
      previously identified electrical engineering design issues.
to quality plant conditions. The team mainly focused on plant systems design and
b.   Observations and Findings
licensing basis requirements issues which were previously identified by the NRC, the
  .1 Undervoltage Time Delay Relay Setting Did Not Account For Instrument
licensee and others during various design reviews conducted in 2002. The team
      Uncertainties
assessed effectiveness of the licensees corrective actions implemented to address
      Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
previously identified electrical engineering design issues.
      "Design Control," having very low safety significance (Green). Specifically, the licensee
  b.
      failed to translate instrument uncertainties into the undervoltage time delay setting
Observations and Findings
      specification for the 4160 Vac buses C1 and D1. Following discovery, the licensee
    .1
      re-evaluated the potential temperature effects to the time delay relays.
Undervoltage Time Delay Relay Setting Did Not Account For Instrument
      Description: The licensee identified in CR 02-05632 that the time delay relays for the
Uncertainties
      59 percent undervoltage condition on 4160 Vac buses C1 and D1 may not have met the
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
      allowable value of 0.5 +/- 0.1 seconds contained in technical specification (TS )
"Design Control," having very low safety significance (Green). Specifically, the licensee
      Table 3.3-4 because instrument uncertainties were not included. The licensee later
failed to translate instrument uncertainties into the undervoltage time delay setting
      initiated CR 03-01448 to specifically determine if the TS value had been exceeded in the
specification for the 4160 Vac buses C1 and D1. Following discovery, the licensee
      past. The licensee determined that the primary cause for fluctuations in the time delays
re-evaluated the potential temperature effects to the time delay relays.
      were temperature variations in the room where the relays were located. The licensee
Description: The licensee identified in CR 02-05632 that the time delay relays for the
      determined that during periods of cool weather, the room would maintain a temperature
59 percent undervoltage condition on 4160 Vac buses C1 and D1 may not have met the
      of approximately 70 degrees Fahrenheit (EF), because the fans in the room would
allowable value of 0.5 +/- 0.1 seconds contained in technical specification (TS )  
      recirculate air from the turbine building to warm the switchgear room when the fan outlet
Table 3.3-4 because instrument uncertainties were not included. The licensee later
      temperature dropped below 70EF. However, the licensee stated that, during the
initiated CR 03-01448 to specifically determine if the TS value had been exceeded in the
      summer, the effects on the time delay relays would be insignificant. Specifically,
past. The licensee determined that the primary cause for fluctuations in the time delays
      CR 03-01448 stated, "Only during summer does the room temperatures increase, and
were temperature variations in the room where the relays were located. The licensee
      even then it does not typically vary during the day. . . Based upon the operation of the
determined that during periods of cool weather, the room would maintain a temperature
                                                28                                      Enclosure
of approximately 70 degrees Fahrenheit (F), because the fans in the room would
recirculate air from the turbine building to warm the switchgear room when the fan outlet
temperature dropped below 70F. However, the licensee stated that, during the
summer, the effects on the time delay relays would be insignificant. Specifically,
CR 03-01448 stated, "Only during summer does the room temperatures increase, and
even then it does not typically vary during the day. . . Based upon the operation of the


Enclosure
29
ventilation system, there is very little potential for the relays to experience a significant
ventilation system, there is very little potential for the relays to experience a significant
temperature rise between the monthly tests."
temperature rise between the monthly tests."
The team questioned this logic, because it was not apparent that temperature effects,
The team questioned this logic, because it was not apparent that temperature effects,
particularly in the summer when outside temperatures could regularly exceed 90EF,
particularly in the summer when outside temperatures could regularly exceed 90F,
would not affect the time delay relays, especially when past experience, which showed
would not affect the time delay relays, especially when past experience, which showed
that some room temperatures could exceed 120EF on hot days, was considered. Based
that some room temperatures could exceed 120F on hot days, was considered. Based
upon the team questions, the licensee re-evaluated the potential temperature effects to
upon the team questions, the licensee re-evaluated the potential temperature effects to
the time delay relays. After performing additional calculations, the licensee determined
the time delay relays. After performing additional calculations, the licensee determined
that increased temperature could cause the time delay to operate outside of its TS
that increased temperature could cause the time delay to operate outside of its TS
limits. Also, the licensee determined that in the past, there was at least one occasion
limits. Also, the licensee determined that in the past, there was at least one occasion
where the temperature in the room was so high that the time delay could have been
where the temperature in the room was so high that the time delay could have been
outside of its TS allowed value. The team was informed by the licensee that, even if the
outside of its TS allowed value. The team was informed by the licensee that, even if the
allowable value requirement had been exceeded, the additional time delay would have
allowable value requirement had been exceeded, the additional time delay would have
had negligible effect on the capability to achieve timely emergency core cooling system
had negligible effect on the capability to achieve timely emergency core cooling system
(ECCS). As the licensee concluded that the relay would have been able to function
(ECCS). As the licensee concluded that the relay would have been able to function
even though it did not meet its TS allowable value, the licensee did not consider the
even though it did not meet its TS allowable value, the licensee did not consider the
relay to have been inoperable. The team did not independently verify this conclusion.
relay to have been inoperable. The team did not independently verify this conclusion.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to translate instrument uncertainty into the specification for undervoltage
licensee failed to translate instrument uncertainty into the specification for undervoltage
time delay relays for the 4160 Vac buses C1 and D1. Since there was a performance
time delay relays for the 4160 Vac buses C1 and D1. Since there was a performance
deficiency, the team compared this performance deficiency to the minor questions
deficiency, the team compared this performance deficiency to the minor questions
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
Reports." The team concluded that the issue was more than minor because this was a
Reports." The team concluded that the issue was more than minor because this was a
design issue which affected the mitigating system cornerstone. The licensee had to
design issue which affected the mitigating system cornerstone. The licensee had to
perform calculations to show that the relays were within the TS allowable values and the
perform calculations to show that the relays were within the TS allowable values and the
licensee determined that the increased temperature could cause the time delay to
licensee determined that the increased temperature could cause the time delay to
operate outside of TS limits. Although the licensee acknowledged that there had been
operate outside of TS limits. Although the licensee acknowledged that there had been
at least one occasion where inclusion of instrument uncertainties into the allowable
at least one occasion where inclusion of instrument uncertainties into the allowable
value would have resulted in an instrument being technically inoperable, the licensee
value would have resulted in an instrument being technically inoperable, the licensee
believed the instrument would still have performed its safety function. Therefore, the
believed the instrument would still have performed its safety function. Therefore, the
licensee did not consider the instrument to have been inoperable. The team reviewed
licensee did not consider the instrument to have been inoperable. The team reviewed
this finding in accordance with IMC 0609, "Significance Determination Process, and
this finding in accordance with IMC 0609, "Significance Determination Process, and
answered no to all five screening questions in the Phase 1 Screening Worksheet
answered no to all five screening questions in the Phase 1 Screening Worksheet
under the Mitigating Systems column. The team concluded the issue was of very low
under the Mitigating Systems column. The team concluded the issue was of very low
safety significance (Green).
safety significance (Green).
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
measures be established to assure that applicable regulatory requirements and the
measures be established to assure that applicable regulatory requirements and the
design basis were correctly translated into specifications, drawings, procedures, and
design basis were correctly translated into specifications, drawings, procedures, and
instructions. Furthermore, it requires that measures be provided for verifying or
instructions. Furthermore, it requires that measures be provided for verifying or
checking the adequacy of design, such as by the performance of design reviews, by the
checking the adequacy of design, such as by the performance of design reviews, by the
use of alternate or simplified calculational methods, or by the performance of a suitable
use of alternate or simplified calculational methods, or by the performance of a suitable
testing program.
testing program.
Contrary to the above, the licensee failed to assure that the regulatory requirements and
Contrary to the above, the licensee failed to assure that the regulatory requirements and
the design basis of the plant were accurately translated into specifications. Specifically,
the design basis of the plant were accurately translated into specifications. Specifically,
the instrument uncertainty was not translated into specification for the undervoltage time
the instrument uncertainty was not translated into specification for the undervoltage time
                                          29                                        Enclosure


  delay relays for the C1 and D1 4160 Vac buses. The licensee had previously entered
Enclosure
  the issue into its CAP as CRs 02-05632 and 03-01448. Because this violation was of
30
  very low safety significance and because it was entered into the licensees CAP, this
delay relays for the C1 and D1 4160 Vac buses. The licensee had previously entered
  violation is being treated as a NCV, consistent with Section VI.A of the NRC
the issue into its CAP as CRs 02-05632 and 03-01448. Because this violation was of
  Enforcement Policy. (NCV 05000346/2003010-03)
very low safety significance and because it was entered into the licensees CAP, this
.2 Lack of 480 Vac Class 1E Motor Thermal Overload Protection
violation is being treated as a NCV, consistent with Section VI.A of the NRC
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
Enforcement Policy. (NCV 05000346/2003010-03)
  having very low safety significance (Green). Specifically, the licensee failed to provide
    .2
  motor thermal overload protection for the Class 1E 480 Vac distribution system.
Lack of 480 Vac Class 1E Motor Thermal Overload Protection
  Following discovery, the licensee physically modified approximately 53 thermal overload
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  circuits to resolve the discrepancy. The primary cause of this violation was related to
having very low safety significance (Green). Specifically, the licensee failed to provide
  the cross-cutting area of human performance because the licensee did not identify the
motor thermal overload protection for the Class 1E 480 Vac distribution system.  
  lack of thermal overload protection was an unanalyzed condition and that the station
Following discovery, the licensee physically modified approximately 53 thermal overload
  was not in compliance with the updated safety analysis report until identified by the
circuits to resolve the discrepancy. The primary cause of this violation was related to
  team.
the cross-cutting area of human performance because the licensee did not identify the
  Description: The team reviewed the design criteria manual for the 480 Vac distribution
lack of thermal overload protection was an unanalyzed condition and that the station
  system. Section 5.4.3.2, "460V Motors Fed from Motor Control Centers," of this design
was not in compliance with the updated safety analysis report until identified by the
  criteria stated that, "Starters should be equipped with overload relays to provide motor
team.
  overload protection. For Class 1E motor operated valves, dampers, pumps, and fans,
Description: The team reviewed the design criteria manual for the 480 Vac distribution
  the thermal overload relays should be bypassed to avoid tripping during emergency
system. Section 5.4.3.2, "460V Motors Fed from Motor Control Centers," of this design
  conditions." This design criteria contradicted Updated Safety Analysis Report (USAR)
criteria stated that, "Starters should be equipped with overload relays to provide motor
  Section 8.3.1.2.11, "Protection Systems," which stated, "Protection systems are
overload protection. For Class 1E motor operated valves, dampers, pumps, and fans,
  provided and designed to initiate automatically the operation of the appropriate
the thermal overload relays should be bypassed to avoid tripping during emergency
  equipment. Necessary protective devices are provided to isolate failed equipment and
conditions." This design criteria contradicted Updated Safety Analysis Report (USAR)
  to identify the equipment that has failed. For the protection system related to
Section 8.3.1.2.11, "Protection Systems," which stated, "Protection systems are
  engineered safety features and essential functions, complete redundancy,
provided and designed to initiate automatically the operation of the appropriate
  independence, and inservice testability is maintained."
equipment. Necessary protective devices are provided to isolate failed equipment and
  The team determined that as a consequence of following the design criteria manual
to identify the equipment that has failed. For the protection system related to
  guidance, the licensee had failed to ensure that the 480V Class 1E circuits were
engineered safety features and essential functions, complete redundancy,
  designed so that the protection systems would automatically initiate appropriate
independence, and inservice testability is maintained."
  equipment, including motor operated valves, dampers, pumps, and fans, as required by
The team determined that as a consequence of following the design criteria manual
  the USAR.
guidance, the licensee had failed to ensure that the 480V Class 1E circuits were
  The team asked the licensee to provide verification that each circuit fed by a Class 1E
designed so that the protection systems would automatically initiate appropriate
  480V motor control center which had its overload protection bypassed or inactivated
equipment, including motor operated valves, dampers, pumps, and fans, as required by
  would be capable of carrying overloads ranging from full load amperes to locked rotor
the USAR.
  amperes on a continuous basis, or until interrupted, without exceeding the ratings of the
The team asked the licensee to provide verification that each circuit fed by a Class 1E
  circuit breaker, the contactor, the bypassed overload device, or the cable. The team
480V motor control center which had its overload protection bypassed or inactivated
  also asked the licensee to assure that when overload protection was bypassed, it did not
would be capable of carrying overloads ranging from full load amperes to locked rotor
  result in jeopardizing the safety function, or in degrading other safety systems.
amperes on a continuous basis, or until interrupted, without exceeding the ratings of the
  As a result of the team's questioning, the licensee identified that, despite the numerous
circuit breaker, the contactor, the bypassed overload device, or the cable. The team
  programmatic design reviews that were completed, engineering had not identified this
also asked the licensee to assure that when overload protection was bypassed, it did not
  discrepancy and there were many circuits where completion of the safety function could
result in jeopardizing the safety function, or in degrading other safety systems.
  not be demonstrated due to bypassing the thermal overload protection. An overload
As a result of the team's questioning, the licensee identified that, despite the numerous
                                            30                                      Enclosure
programmatic design reviews that were completed, engineering had not identified this
discrepancy and there were many circuits where completion of the safety function could
not be demonstrated due to bypassing the thermal overload protection. An overload


Enclosure
31
condition in a single circuit could result in opening of the upstream circuit breaker to the
condition in a single circuit could result in opening of the upstream circuit breaker to the
bus, thus removing 480V power to all other Class 1E equipment connected to that bus.
bus, thus removing 480V power to all other Class 1E equipment connected to that bus.  
The team also identified additional bypassing of thermal overload protection on Class 1E
The team also identified additional bypassing of thermal overload protection on Class 1E
480V loads, where the design criteria did not allow such bypassing.
480V loads, where the design criteria did not allow such bypassing.
The licensee characterized this issue as having "potential for a significant impact on
The licensee characterized this issue as having "potential for a significant impact on
safety" and wrote numerous CRs to address the issue. Subsequently, the licensee
safety" and wrote numerous CRs to address the issue. Subsequently, the licensee
modified approximately 53 thermal overload circuits as part of the issue resolution.
modified approximately 53 thermal overload circuits as part of the issue resolution.  
There was reasonable assurance that the condition did not result in a loss of system
There was reasonable assurance that the condition did not result in a loss of system
function
function  
During review of this issue, the team also noted an example of an ineffective roll-over in
During review of this issue, the team also noted an example of an ineffective roll-over in
that some of the concerns identified in CR 03-02616 were rolled over to CR 03-03572
that some of the concerns identified in CR 03-02616 were rolled over to CR 03-03572
and were not adequately addressed. The team was concerned about this issue
and were not adequately addressed. The team was concerned about this issue
because it had occurred after the licensee had revised its roll-over process to address
because it had occurred after the licensee had revised its roll-over process to address
concerns expressed by the team earlier in the inspection.
concerns expressed by the team earlier in the inspection.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to provide protective devices, such as thermal overloads, for 480V Class
licensee failed to provide protective devices, such as thermal overloads, for 480V Class
1E circuits as specified in design documents. Since there was a performance
1E circuits as specified in design documents. Since there was a performance
deficiency, the team compared this performance deficiency to the minor questions
deficiency, the team compared this performance deficiency to the minor questions
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
Reports." The team concluded that the issue was more than minor because this was a
Reports." The team concluded that the issue was more than minor because this was a
design issue which affected the mitigating systems cornerstone. The licensee failed to
design issue which affected the mitigating systems cornerstone. The licensee failed to
ensure that bypassing the thermal overload protection would result in completion of
ensure that bypassing the thermal overload protection would result in completion of
safety functions and subsequently had to install thermal overload protection in order to
safety functions and subsequently had to install thermal overload protection in order to
meet the design requirements. The team reviewed this finding in accordance with IMC
meet the design requirements. The team reviewed this finding in accordance with IMC
0609, "Significance Determination Process, and answered no to all five screening
0609, "Significance Determination Process, and answered no to all five screening
questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.
questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.  
The team concluded the issue was of very low safety significance (Green).
The team concluded the issue was of very low safety significance (Green).
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
measures be established to assure that applicable regulatory requirements and the
measures be established to assure that applicable regulatory requirements and the
design basis are correctly translated into specifications, drawings, procedures, and
design basis are correctly translated into specifications, drawings, procedures, and
instructions. USAR Section 8.3.1.2.11, "Protection Systems," stated, in part, that,
instructions. USAR Section 8.3.1.2.11, "Protection Systems," stated, in part, that,
protective devices are provided to isolate failed equipment and to identify the equipment
protective devices are provided to isolate failed equipment and to identify the equipment
that has failed. Furthermore, for the protection system related to engineered safety
that has failed. Furthermore, for the protection system related to engineered safety
features and essential functions, complete redundancy, independence, and inservice
features and essential functions, complete redundancy, independence, and inservice
testability is maintained.
testability is maintained.
Contrary to the above, the licensee failed to correctly translate the design basis into
Contrary to the above, the licensee failed to correctly translate the design basis into
specifications. Specifically, the licensee failed to provide the necessary protective
specifications. Specifically, the licensee failed to provide the necessary protective
devices, such as thermal overload protection for the for 480V Class 1E circuits. The
devices, such as thermal overload protection for the for 480V Class 1E circuits. The
protection was required to isolate failed equipment and limit fault propagation. The
protection was required to isolate failed equipment and limit fault propagation. The
licensee entered the issue into its CAP as CRs 03-02597, 03-02616, 03-03572,
licensee entered the issue into its CAP as CRs 03-02597, 03-02616, 03-03572,
03-04264, 03-04303, 03-04375, 03-06475, 03-06567 and 03-07031. Because this
03-04264, 03-04303, 03-04375, 03-06475, 03-06567 and 03-07031. Because this
violation was of very low safety significance and because it was entered into the
violation was of very low safety significance and because it was entered into the
licensees CAP, the violation is being treated as a NCV, consistent with Section VI.A of
licensees CAP, the violation is being treated as a NCV, consistent with Section VI.A of
the NRC Enforcement Policy. (NCV 05000346/2003010-04)
the NRC Enforcement Policy. (NCV 05000346/2003010-04)
                                          31                                      Enclosure


.3 Failure to Perform Direct Current Contactor Testing to Ensure Minimum Voltage
Enclosure
  at Motor Operated Valves
32
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,
    .3
  Test Control, having very low safety significance (Green). Specifically, the licensee
Failure to Perform Direct Current Contactor Testing to Ensure Minimum Voltage
  failed to adequately test direct current (DC) contactors related to two safety related
at Motor Operated Valves
  motor operated steam valves associated with the AFW system. Following discovery, the
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,
  licensee entered the issue into the corrective action program and was re-evaluating the
Test Control, having very low safety significance (Green). Specifically, the licensee
  basis for acceptability of these valves. The primary cause of this violation was related to
failed to adequately test direct current (DC) contactors related to two safety related
  the cross-cutting area of problem identification and resolution because, although the
motor operated steam valves associated with the AFW system. Following discovery, the
  issue was identified in 2002, the licensee did not take corrective action until prompted by
licensee entered the issue into the corrective action program and was re-evaluating the
  the team in 2003.
basis for acceptability of these valves. The primary cause of this violation was related to
  Description: The team reviewed CR 01-03059,which documented the issue of minimum
the cross-cutting area of problem identification and resolution because, although the
  voltage available at two safety related motor operated steam valves associated with the
issue was identified in 2002, the licensee did not take corrective action until prompted by
  AFW system. One of the valves was normally closed and was required to be opened
the team in 2003.
  under certain conditions to allow the AFW system to perform its intended function. It
Description: The team reviewed CR 01-03059,which documented the issue of minimum
  had a cable conductor circuit length of 6,814 feet for the automatic opening function.
voltage available at two safety related motor operated steam valves associated with the
  The licensees corrective action to the issue was to revise calculation C-EE-002.02-010
AFW system. One of the valves was normally closed and was required to be opened
  to include the valves which had not been previously addressed in the calculation. This
under certain conditions to allow the AFW system to perform its intended function. It
  corrective action was implemented in April 2002. In review of the calculation, the team
had a cable conductor circuit length of 6,814 feet for the automatic opening function.  
  noted that Attachment 27 of the calculation included the test data used to establish a
The licensees corrective action to the issue was to revise calculation C-EE-002.02-010
  minimum voltage for the DC contactors. The team ascertained that the testing was
to include the valves which had not been previously addressed in the calculation. This
  based on a single device and lacked sufficient basis to conclude that other contactors
corrective action was implemented in April 2002. In review of the calculation, the team
  would actuate under similar conditions. In addition, the test used an uncalibrated meter
noted that Attachment 27 of the calculation included the test data used to establish a
  to collect data. The team also noted that no adjustment had been made to factor plant
minimum voltage for the DC contactors. The team ascertained that the testing was
  environmental conditions into the results. The licensee issued CR 03-07069 during the
based on a single device and lacked sufficient basis to conclude that other contactors
  inspection to document this deficiency in testing methodology.
would actuate under similar conditions. In addition, the test used an uncalibrated meter
  As a result of the deficiencies in the testing methodology, the team could not conclude
to collect data. The team also noted that no adjustment had been made to factor plant
  that the valves had sufficient minimum voltage at the component to perform their safety
environmental conditions into the results. The licensee issued CR 03-07069 during the
  function. The team also noted that the licensee's evaluation of the team-identified
inspection to document this deficiency in testing methodology.
  deficiency was that it was acceptable because of the single failure criteria (i.e., that even
As a result of the deficiencies in the testing methodology, the team could not conclude
  if one valve failed, the other train would be available because the single failure had
that the valves had sufficient minimum voltage at the component to perform their safety
  already occurred). The team informed the licensee that this appeared to be an
function. The team also noted that the licensee's evaluation of the team-identified
  inappropriate application of the single failure criteria.
deficiency was that it was acceptable because of the single failure criteria (i.e., that even
  Analysis: The team determined that a performance deficiency existed because the
if one valve failed, the other train would be available because the single failure had
  licensee failed to ensure proper testing of DC contactors. Since there was a
already occurred). The team informed the licensee that this appeared to be an
  performance deficiency, the team compared this performance deficiency to the minor
inappropriate application of the single failure criteria.
  questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
Analysis: The team determined that a performance deficiency existed because the
  Inspection Reports." The team concluded that the issue was more than minor because
licensee failed to ensure proper testing of DC contactors. Since there was a
  the licensee had relied upon an inadequate test to demonstrate that the contactors were
performance deficiency, the team compared this performance deficiency to the minor
  qualified to perform under required conditions and because the contactors were installed
questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
  in the plant during previous operating cycles. The licensee determined that the valves
Inspection Reports." The team concluded that the issue was more than minor because
  had always been operable. This was a design qualification issue which affected the
the licensee had relied upon an inadequate test to demonstrate that the contactors were
  mitigating systems cornerstone. The team reviewed this finding in accordance with IMC
qualified to perform under required conditions and because the contactors were installed
  0609, "Significance Determination Process, and answered no to all five screening
in the plant during previous operating cycles. The licensee determined that the valves
                                            32                                      Enclosure
had always been operable. This was a design qualification issue which affected the
mitigating systems cornerstone. The team reviewed this finding in accordance with IMC
0609, "Significance Determination Process, and answered no to all five screening


  questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.
Enclosure
  The team concluded the issue was of very low safety significance (Green).
33
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI requires, in part, that a test
questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.  
  program shall be established to assure that all testing required to demonstrate that
The team concluded the issue was of very low safety significance (Green).
  structures, systems, and components will perform satisfactorily in service is identified
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI requires, in part, that a test
  and performed in accordance with written procedures. Test procedures shall include
program shall be established to assure that all testing required to demonstrate that
  provisions for assuring that all prerequisites for the given test have been met, that
structures, systems, and components will perform satisfactorily in service is identified
  adequate test instrumentation is available and used, and that the test is performed
and performed in accordance with written procedures. Test procedures shall include
  under suitable environmental conditions.
provisions for assuring that all prerequisites for the given test have been met, that
  Contrary to the above, during the testing for establishing a minimum voltage for DC
adequate test instrumentation is available and used, and that the test is performed
  contactors, the licensee failed to: ensure the components would perform satisfactorily in
under suitable environmental conditions.
  service; failed to use adequate test instrumentation; and failed to ensure the test was
Contrary to the above, during the testing for establishing a minimum voltage for DC
  performed under suitable environmental conditions. Specifically, the licensee used a
contactors, the licensee failed to: ensure the components would perform satisfactorily in
  sample size of one DC contactor to justify pick-up voltages of other DC contactors in the
service; failed to use adequate test instrumentation; and failed to ensure the test was
  plant. In addition, the licensee used uncalibrated instrumentation and failed to consider
performed under suitable environmental conditions. Specifically, the licensee used a
  actual plant environment to which the DC contactors would be subject.
sample size of one DC contactor to justify pick-up voltages of other DC contactors in the
  The licensee entered the issue into its CAP as CR 03-07069. Because this violation
plant. In addition, the licensee used uncalibrated instrumentation and failed to consider
  was of very low safety significance and because it was entered into the licensees CAP,
actual plant environment to which the DC contactors would be subject.
  the violation is being treated as a NCV, consistent with Section VI.A of the NRC
The licensee entered the issue into its CAP as CR 03-07069. Because this violation
  Enforcement Policy. (NCV 05000346/2003010-05)
was of very low safety significance and because it was entered into the licensees CAP,
.4 Failure to Verify Adequacy of Short Circuit Protection for Direct Current Circuits
the violation is being treated as a NCV, consistent with Section VI.A of the NRC
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
Enforcement Policy. (NCV 05000346/2003010-05)
  "Corrective Action," having very low safety significance (Green). Specifically, the
    .4
  licensee failed to identify and correct inadequate short circuit protection for DC circuits.
Failure to Verify Adequacy of Short Circuit Protection for Direct Current Circuits
  Following discovery, the licensee issued Condition Report 03-06944 to document the
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
  deficient circuit protection for valves having extremely long circuit lengths. The primary
"Corrective Action," having very low safety significance (Green). Specifically, the
  cause of this violation was related to the cross-cutting area of problem identification and
licensee failed to identify and correct inadequate short circuit protection for DC circuits.  
  resolution because the licensee had missed several opportunities to identify it as part of
Following discovery, the licensee issued Condition Report 03-06944 to document the
  corrective actions for previously identified DC circuit deficiencies.
deficient circuit protection for valves having extremely long circuit lengths. The primary
  Description: While reviewing CRs 01-03059 and 02-00412 and calculation
cause of this violation was related to the cross-cutting area of problem identification and
  C-EE-002.01-010, the team questioned the adequacy of DC circuit protection for long
resolution because the licensee had missed several opportunities to identify it as part of
  DC circuits, such as the one described in Section 4OA3(2)b.3, which had a cable
corrective actions for previously identified DC circuit deficiencies.
  conductor circuit length of 6,814 feet. Subsequently, the licensee evaluated the
Description: While reviewing CRs 01-03059 and 02-00412 and calculation
  adequacy of the fuse sizing and identified that, in the case of short circuits, the circuit
C-EE-002.01-010, the team questioned the adequacy of DC circuit protection for long
  resistance could be high enough to preclude operation of the fuses protecting circuit,
DC circuits, such as the one described in Section 4OA3(2)b.3, which had a cable
  i.e., the fuses protecting the circuits were oversized for the application. Thus, a short
conductor circuit length of 6,814 feet. Subsequently, the licensee evaluated the
  circuit current could be allowed to flow for an indeterminate length of time. The short
adequacy of the fuse sizing and identified that, in the case of short circuits, the circuit
  circuit current would only be interrupted after considerable damage had been made to
resistance could be high enough to preclude operation of the fuses protecting circuit,
  safety related equipment and could result in damaging fires which could affect
i.e., the fuses protecting the circuits were oversized for the application. Thus, a short
  redundant safety related trains. The licensee issued CR 03-06944 to document the
circuit current could be allowed to flow for an indeterminate length of time. The short
  deficient circuit protection for valves having extremely long circuit lengths. Subsequent
circuit current would only be interrupted after considerable damage had been made to
  to the inspection, the licensee developed an engineering package to replace the fuses in
safety related equipment and could result in damaging fires which could affect
  March 2004. The inspectors reviewed the licensees engineering package and
redundant safety related trains. The licensee issued CR 03-06944 to document the
                                            33                                      Enclosure
deficient circuit protection for valves having extremely long circuit lengths. Subsequent
to the inspection, the licensee developed an engineering package to replace the fuses in
March 2004. The inspectors reviewed the licensees engineering package and


  concluded that the projected completion date appears reasonable and commensurate
Enclosure
  with the safety significance of the issue.
34
  Analysis: The team determined that a performance deficiency existed because the
concluded that the projected completion date appears reasonable and commensurate
  licensee failed to verify the adequacy of short circuit protection for DC circuits. Since
with the safety significance of the issue.
  there was a performance deficiency, the team compared this performance deficiency to
Analysis: The team determined that a performance deficiency existed because the
  the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
licensee failed to verify the adequacy of short circuit protection for DC circuits. Since
  Reactor Inspection Reports." The team concluded that the issue was more than minor
there was a performance deficiency, the team compared this performance deficiency to
  because the licensee had to perform calculations to determine if the fuses would
the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
  adequately protect the equipment and because modifications to those fuses were
Reactor Inspection Reports." The team concluded that the issue was more than minor
  required. This was a design issue which affected the mitigating systems cornerstone.
because the licensee had to perform calculations to determine if the fuses would
  The team reviewed this finding in accordance with IMC 0609, "Significance Determination
adequately protect the equipment and because modifications to those fuses were
  Process, and answered no to all five screening questions in the Phase 1 Screening
required. This was a design issue which affected the mitigating systems cornerstone.  
  Worksheet under the Mitigating Systems column. The team concluded the issue was of
The team reviewed this finding in accordance with IMC 0609, "Significance Determination
  very low safety significance (Green).
Process, and answered no to all five screening questions in the Phase 1 Screening
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI requires, in part, that
Worksheet under the Mitigating Systems column. The team concluded the issue was of
  conditions adverse to quality be promptly identified and corrected.
very low safety significance (Green).
  Contrary to the above, as of August 25, 2003, the licensee did not promptly identify and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI requires, in part, that
  correct a condition adverse to quality in that DC circuits were not adequately protected
conditions adverse to quality be promptly identified and corrected.
  against short circuits, a condition adverse to quality. Specifically, the licensee missed
Contrary to the above, as of August 25, 2003, the licensee did not promptly identify and
  several opportunities in 2001 and 2002 to identify that there was no basis ensuring
correct a condition adverse to quality in that DC circuits were not adequately protected
  adequate short circuit protection for DC circuits and did not initiate corrective actions to
against short circuits, a condition adverse to quality. Specifically, the licensee missed
  ensure that fuse sizing was adequate for long DC circuits such as those for motor
several opportunities in 2001 and 2002 to identify that there was no basis ensuring
  operated valves MV0106 and MV3870. The licensee entered this issue into its
adequate short circuit protection for DC circuits and did not initiate corrective actions to
  corrective action as CR 03-06944. Because this violation was of very low safety
ensure that fuse sizing was adequate for long DC circuits such as those for motor
  significance and because it was entered into the licensees CAP, this violation is being
operated valves MV0106 and MV3870. The licensee entered this issue into its
  treated as a NCV, consistent with Section VI.A of the NRC Enforcement Policy.
corrective action as CR 03-06944. Because this violation was of very low safety
  (NCV 05000346/2003010-06)
significance and because it was entered into the licensees CAP, this violation is being
.5 Lack of Calculations to Ensure Minimum Voltage Availability at Device Terminals
treated as a NCV, consistent with Section VI.A of the NRC Enforcement Policy.  
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
(NCV 05000346/2003010-06)
  having very low safety significance (Green). Specifically, the licensee failed to confirm
    .5
  operability of DC contactors by ensuring that minimum voltage was available at the
Lack of Calculations to Ensure Minimum Voltage Availability at Device Terminals
  safety related device terminals. The licensee missed several opportunities to correct
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  this design deficiency. Following discovery, the licensee issued Condition Report
having very low safety significance (Green). Specifically, the licensee failed to confirm
  03-06956 and evaluated the issue. The primary cause of this violation was related to
operability of DC contactors by ensuring that minimum voltage was available at the
  the cross-cutting area of problem identification and resolution because, although the
safety related device terminals. The licensee missed several opportunities to correct
  issue was identified in 2002, the licensee failed to take appropriate corrective action to
this design deficiency. Following discovery, the licensee issued Condition Report
  thoroughly evaluate the problem until prompted by the team in 2003.
03-06956 and evaluated the issue. The primary cause of this violation was related to
  Description: As a part of CR 01-03059, the licensee performed an extent of condition
the cross-cutting area of problem identification and resolution because, although the
  evaluation and identified that the DC voltages in calculation C-EE-002.01-010 evaluated
issue was identified in 2002, the licensee failed to take appropriate corrective action to
  available voltage to the panel terminals only. The calculation did not confirm sufficient
thoroughly evaluate the problem until prompted by the team in 2003.
  voltage at device terminal for proper operation. The licensee issued CR 02-00412 to
Description: As a part of CR 01-03059, the licensee performed an extent of condition
  document this deficiency. In response to this CR, the licensee issued a revision to the
evaluation and identified that the DC voltages in calculation C-EE-002.01-010 evaluated
  calculation.
available voltage to the panel terminals only. The calculation did not confirm sufficient
                                            34                                        Enclosure
voltage at device terminal for proper operation. The licensee issued CR 02-00412 to
document this deficiency. In response to this CR, the licensee issued a revision to the
calculation.


Enclosure
35
During review of calculation C-EE-002.01-010, the team determined that the lowest
During review of calculation C-EE-002.01-010, the team determined that the lowest
voltage was 106.38V, which would occur during the first one minute discharge period.
voltage was 106.38V, which would occur during the first one minute discharge period.  
The calculation was potentially non-conservative because it failed to address resistance
The calculation was potentially non-conservative because it failed to address resistance
of contacts and fuses which would contribute to additional voltage drop in the circuits.
of contacts and fuses which would contribute to additional voltage drop in the circuits.  
Conservatism existed in the calculation since all loads were assumed to run
Conservatism existed in the calculation since all loads were assumed to run
continuously and simultaneously during the first minute of battery discharge. Additional
continuously and simultaneously during the first minute of battery discharge. Additional
conservatism was identified during service testing of the battery with the plant
conservatism was identified during service testing of the battery with the plant
anticipated loads. Nevertheless, the team could not conclude that the conservatism was
anticipated loads. Nevertheless, the team could not conclude that the conservatism was
sufficient to bound the undetermined voltage drop in part of the circuits. Therefore, it
sufficient to bound the undetermined voltage drop in part of the circuits. Therefore, it
was not known whether the device terminal voltage present under the design basis
was not known whether the device terminal voltage present under the design basis
conditions would be sufficient to ensure proper operation of safety related devices.
conditions would be sufficient to ensure proper operation of safety related devices.
Line 2,021: Line 2,358:
calculation, the licensee identified a potential SCAQ because potential operability
calculation, the licensee identified a potential SCAQ because potential operability
concerns were raised that could have affected numerous pieces of safety related
concerns were raised that could have affected numerous pieces of safety related
equipment, the licensee did not take actions to ensure operability. Specifically, the
equipment, the licensee did not take actions to ensure operability. Specifically, the
licensee did not have a documented basis for resolving the operability concern for
licensee did not have a documented basis for resolving the operability concern for
equipment which might not have sufficient voltages to ensure proper operation. The CR
equipment which might not have sufficient voltages to ensure proper operation. The CR
stated that, "preliminary reviews indicate that there are no operability concerns" and the
stated that, "preliminary reviews indicate that there are no operability concerns" and the
due date for the corrective action to evaluate the loads connected to the panels was
due date for the corrective action to evaluate the loads connected to the panels was
assigned as a post-restart action. After the operability issue was raised by the team, the
assigned as a post-restart action. After the operability issue was raised by the team, the
licensee issued CR 03-06956 for the lack of basis for deferring corrective action. The
licensee issued CR 03-06956 for the lack of basis for deferring corrective action. The
licensee performed additional analysis and extent of condition reviews. The licensee
licensee performed additional analysis and extent of condition reviews. The licensee
determined that there were no operability issues based on the results of the re-analysis.
determined that there were no operability issues based on the results of the re-analysis.  
The team reviewed these re-analyses and concluded there is reasonable assurance that
The team reviewed these re-analyses and concluded there is reasonable assurance that
the affected components are operable.
the affected components are operable.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to ensure the availability of minimum voltage at the safety related device
licensee failed to ensure the availability of minimum voltage at the safety related device
terminals. Specifically, the licensee had not performed design analyses or calculations
terminals. Specifically, the licensee had not performed design analyses or calculations
to demonstrate that end devices would have sufficient voltage available to perform the
to demonstrate that end devices would have sufficient voltage available to perform the
design function. Since there was a performance deficiency, the team compared this
design function. Since there was a performance deficiency, the team compared this
performance deficiency to the minor questions contained in Appendix B, "Issue
performance deficiency to the minor questions contained in Appendix B, "Issue
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
that the issue was more than minor because the licensee had to perform calculations to
that the issue was more than minor because the licensee had to perform calculations to
demonstrate that the devices had sufficient voltage to perform their safety function.
demonstrate that the devices had sufficient voltage to perform their safety function.  
Based on the evaluation performed as a corrective action to CR 03-06956, the team had
Based on the evaluation performed as a corrective action to CR 03-06956, the team had
reasonable assurance that affected components were operable. This was a design
reasonable assurance that affected components were operable. This was a design
issue which affected the mitigating systems cornerstone. The team reviewed this
issue which affected the mitigating systems cornerstone. The team reviewed this
finding in accordance with IMC 0609, "Significance Determination Process, and
finding in accordance with IMC 0609, "Significance Determination Process, and
answered no to all five screening questions in the Phase 1 Screening Worksheet
answered no to all five screening questions in the Phase 1 Screening Worksheet
under the Mitigating Systems column. The team concluded the issue was of very low
under the Mitigating Systems column. The team concluded the issue was of very low
safety significance (Green).
safety significance (Green).
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III requires, in part, that
measures be established to assure that applicable regulatory requirements and the
measures be established to assure that applicable regulatory requirements and the
design basis are correctly translated into specifications, drawings, procedures, and
design basis are correctly translated into specifications, drawings, procedures, and
instructions. measures be established to assure that applicable regulatory requirements
instructions. measures be established to assure that applicable regulatory requirements
and the design basis were correctly translated into specifications, drawings, procedures,
and the design basis were correctly translated into specifications, drawings, procedures,
                                          35                                      Enclosure


  and instructions. Furthermore, it requires that measures be provided for verifying or
Enclosure
  checking the adequacy of design, such as by the performance of design reviews, by the
36
  use of alternate or simplified calculational methods, or by the performance of a suitable
and instructions. Furthermore, it requires that measures be provided for verifying or
  testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
  Contrary to the above, the licensee had failed to ensure that minimum voltage would be
use of alternate or simplified calculational methods, or by the performance of a suitable
  available at the safety related device terminals. The calculation performed by the
testing program.
  licensee did not confirm that sufficient voltage would exist at the device terminals for
Contrary to the above, the licensee had failed to ensure that minimum voltage would be
  proper operation of safety related components during design basis events. The licensee
available at the safety related device terminals. The calculation performed by the
  issued CR 03-06956 to address this deficiency. Because this violation was of very low
licensee did not confirm that sufficient voltage would exist at the device terminals for
  safety significance and because it was entered into the licensees CAP, this violation is
proper operation of safety related components during design basis events. The licensee
  being treated as a NCV consistent with Section VI.A of the NRC Enforcement Policy.
issued CR 03-06956 to address this deficiency. Because this violation was of very low
  (NCV 05000346/2003010-07)
safety significance and because it was entered into the licensees CAP, this violation is
.6 Raychem' Splice Removal on Containment Air Cooler Motor Cables
being treated as a NCV consistent with Section VI.A of the NRC Enforcement Policy.  
  Introduction: The team identified a performance deficiency involving the failure to
(NCV 05000346/2003010-07)
  properly remove Raychem' splices during the CACs motor replacement. Following
    .6
  discovery, the licensee entered the issue into its corrective action process. After NRC
Raychem' Splice Removal on Containment Air Cooler Motor Cables
  identified the cause of the condition, the licensee took corrective actions. This was a
Introduction: The team identified a performance deficiency involving the failure to
  minor violation.
properly remove Raychem' splices during the CACs motor replacement. Following
  Description: During CAC motor replacement, the licensee identified splitting of the
discovery, the licensee entered the issue into its corrective action process. After NRC
  motor cable insulation as documented in CR 02-05459. The cable jacket and insulation
identified the cause of the condition, the licensee took corrective actions. This was a
  to the three CAC motor high speed windings were found to be split at the ends which
minor violation.
  were normally covered by Raychem' heat shrink sleeves. The damage was observed
Description: During CAC motor replacement, the licensee identified splitting of the
  after the Raychem' sleeves were removed for de-terminating the motors. In 2002, the
motor cable insulation as documented in CR 02-05459. The cable jacket and insulation
  NRC examined this issue and concluded that the CAC cable had apparently been cut by
to the three CAC motor high speed windings were found to be split at the ends which
  a sharp instrument, rather than the result of an aging or contamination related
were normally covered by Raychem' heat shrink sleeves. The damage was observed
  mechanism as initially assumed by the licensee. The NRC determined that the splitting
after the Raychem' sleeves were removed for de-terminating the motors. In 2002, the
  was in fact a deep gash and the licensee subsequently determined the gash was
NRC examined this issue and concluded that the CAC cable had apparently been cut by
  inflicted by a contractor when removing the Raychem' sleeves with a knife. To
a sharp instrument, rather than the result of an aging or contamination related
  address this concern, the licensee initiated work orders to replace the section of the high
mechanism as initially assumed by the licensee. The NRC determined that the splitting
  speed cable of the three CAC motors between the motor and the penetrations with an
was in fact a deep gash and the licensee subsequently determined the gash was
  equivalent cable. The work procedures were revised, and the workers received training
inflicted by a contractor when removing the Raychem' sleeves with a knife. To
  on the revised procedures.
address this concern, the licensee initiated work orders to replace the section of the high
  The approved method for removal of Raychem' sleeves was prescribed in
speed cable of the three CAC motors between the motor and the penetrations with an
  maintenance procedure DB-ME-09500, "Installation and Termination of Electrical
equivalent cable. The work procedures were revised, and the workers received training
  Cables," which required that Raychem' sleeves be removed by lightly scoring the
on the revised procedures.
  sleeve with a knife and then applying heat to remove the sleeve. During the licensee
The approved method for removal of Raychem' sleeves was prescribed in
  investigation of the issue, the contractor performing this activity stated that he was not
maintenance procedure DB-ME-09500, "Installation and Termination of Electrical
  trained on the Raychem' removal technique and was not aware of the applicable
Cables," which required that Raychem' sleeves be removed by lightly scoring the
  procedure. However, the licensees cause analysis determined that the contractor
sleeve with a knife and then applying heat to remove the sleeve. During the licensee
  performing the task had been trained and qualified. Nevertheless, the contractor did not
investigation of the issue, the contractor performing this activity stated that he was not
  perform the Raychem' sleeve removal in accordance with appropriate and applicable
trained on the Raychem' removal technique and was not aware of the applicable
  procedures. At the time of the inspection, the team noted that the licensee had not
procedure. However, the licensees cause analysis determined that the contractor
  documented whether an extent-of-condition review was performed to determine if other
performing the task had been trained and qualified. Nevertheless, the contractor did not
  maintenance activities were incorrectly performed. On March 2, 2004, the licensee
perform the Raychem' sleeve removal in accordance with appropriate and applicable
                                            36                                      Enclosure
procedures. At the time of the inspection, the team noted that the licensee had not
documented whether an extent-of-condition review was performed to determine if other
maintenance activities were incorrectly performed. On March 2, 2004, the licensee


  informed the team that the individual had not removed any other Raychem' splices in
Enclosure
  the past and the subject work activity was limited to this individual only.
37
  Analysis: The team determined that a performance deficiency existed because the
informed the team that the individual had not removed any other Raychem' splices in
  licensee failed to follow the maintenance procedure for removing Raychem' sleeves.
the past and the subject work activity was limited to this individual only.
  Since there was a performance deficiency, the team compared this performance
Analysis: The team determined that a performance deficiency existed because the
  deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
licensee failed to follow the maintenance procedure for removing Raychem' sleeves.  
  0612, "Power Reactor Inspection Reports." The team concluded that the issue was
Since there was a performance deficiency, the team compared this performance
  minor because it was identified while the system was out of service, and it was corrected
deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
  before the system was returned to service.
0612, "Power Reactor Inspection Reports." The team concluded that the issue was
  Enforcement: The failure to follow the maintenance procedure for removing Raychem'
minor because it was identified while the system was out of service, and it was corrected
  sleeves constituted a violation of 10 CFR Appendix B, Criterion V, which has minor
before the system was returned to service.
  significance and is not subject to enforcement action in accordance with Section IV of
Enforcement: The failure to follow the maintenance procedure for removing Raychem'
  the NRCs Enforcement Policy. The licensee entered the issue into its CAP as
sleeves constituted a violation of 10 CFR Appendix B, Criterion V, which has minor
  CR 02-05459.
significance and is not subject to enforcement action in accordance with Section IV of
  While minor violations are not normally documented in inspection reports, the team
the NRCs Enforcement Policy. The licensee entered the issue into its CAP as
  determined that documentation was appropriate in this case since the licensee had not
CR 02-05459.  
  documented whether any extent-of-condition review had been performed and the
While minor violations are not normally documented in inspection reports, the team
  underlying cause is similar to that of other findings in this report.
determined that documentation was appropriate in this case since the licensee had not
.7 Review of Calculation on the Electric Transient Analysis Profile
documented whether any extent-of-condition review had been performed and the
  Introduction: The team reviewed ETAP calculation C-EE-015.03-008, Revision 2, to
underlying cause is similar to that of other findings in this report.
  evaluate technical adequacy.
    .7
  Description: A third revision to the calculation was under way during the inspection and
Review of Calculation on the Electric Transient Analysis Profile
  was not scheduled to be completed until after the inspection was over. The fact that the
Introduction: The team reviewed ETAP calculation C-EE-015.03-008, Revision 2, to
  licensee was continuing to revise the calculation hampered the team's overall ability to
evaluate technical adequacy.
  assess its acceptability. However, the calculation appeared to be generally well
Description: A third revision to the calculation was under way during the inspection and
  performed and did successfully resolve a multitude of issues. The licensee also
was not scheduled to be completed until after the inspection was over. The fact that the
  performed a very good self-assessment with an industry group comprised of outside
licensee was continuing to revise the calculation hampered the team's overall ability to
  independent consultants. However, the team considered the ETAP calculation
assess its acceptability. However, the calculation appeared to be generally well
  development to be very slow in regards to implementation of corrective actions. For
performed and did successfully resolve a multitude of issues. The licensee also
  example, changes in auto transfer functions and the EDG calculation which were
performed a very good self-assessment with an industry group comprised of outside
  completed in January 2003 had not yet been incorporated into the main ETAP
independent consultants. However, the team considered the ETAP calculation
  calculation. The team also observed that the calculation was performed by contractors
development to be very slow in regards to implementation of corrective actions. For
  and that the licensee's internal knowledge of the calculation appeared limited.
example, changes in auto transfer functions and the EDG calculation which were
  Analysis: As a minor issue, the team noted that procedure NOP-CC-3002 required that
completed in January 2003 had not yet been incorporated into the main ETAP
  calculations be entered into the calculation database prior to issuing of a new revision.
calculation. The team also observed that the calculation was performed by contractors
  However, the team identified that document control was not notified upon issuance of a
and that the licensee's internal knowledge of the calculation appeared limited.
  new revision to calculation C-EE-015.03-008 (Revision 2).
Analysis: As a minor issue, the team noted that procedure NOP-CC-3002 required that
  Enforcement: The failure to enter the revision of a procedure into the database prior to
calculations be entered into the calculation database prior to issuing of a new revision.  
  its issuance constitutes a violation of minor significance that is not subject to
However, the team identified that document control was not notified upon issuance of a
  enforcement action in accordance with Section IV of the NRCs Enforcement Policy.
new revision to calculation C-EE-015.03-008 (Revision 2).
  The licensee documented the issue in CR 03-06989.
Enforcement: The failure to enter the revision of a procedure into the database prior to
                                            37                                      Enclosure
its issuance constitutes a violation of minor significance that is not subject to
enforcement action in accordance with Section IV of the NRCs Enforcement Policy.  
The licensee documented the issue in CR 03-06989.


  While minor violations are not normally documented in inspection reports, the team
Enclosure
  determined that documentation was appropriate in this case it represented an example
38
  of calculation weakness and the underlying cause is similar to that of other findings in
While minor violations are not normally documented in inspection reports, the team
  this report.
determined that documentation was appropriate in this case it represented an example
.8 Inadequate Grid Voltage Calculations
of calculation weakness and the underlying cause is similar to that of other findings in
  Introduction: The team identified that the licensee failed to consider the worst case grid
this report.
  voltages in the short circuit analyses. Following discovery, the licensee entered the
    .8
  issue into their corrective action program and performed new calculations to address the
Inadequate Grid Voltage Calculations
  issue.
Introduction: The team identified that the licensee failed to consider the worst case grid
  Description: The licensee initiated CR 02-06302 to document that the licensee had not
voltages in the short circuit analyses. Following discovery, the licensee entered the
  considered the worst case grid voltage. This CR described the issue as being
issue into their corrective action program and performed new calculations to address the
  administrative in nature and having no effect on the results. This conclusion was
issue.
  incorrect and was so recognized in CR 02-06837.
Description: The licensee initiated CR 02-06302 to document that the licensee had not
  The team ascertained that the maximum grid voltage was an important parameter which
considered the worst case grid voltage. This CR described the issue as being
  affected the accuracy of the short circuit calculations. The postulated short circuit
administrative in nature and having no effect on the results. This conclusion was
  current would proportionally increase for higher grid voltage, therefore, calculations
incorrect and was so recognized in CR 02-06837.
  performed for lower grid voltages would be non-conservative. The team reviewed this
The team ascertained that the maximum grid voltage was an important parameter which
  item and determined that calculation C-EE-015.03-003 was superseded with calculation
affected the accuracy of the short circuit calculations. The postulated short circuit
  C-EE-015.03-008, which utilized the ETAP program described in Section 4OA3(2)b.7.
current would proportionally increase for higher grid voltage, therefore, calculations
  The new calculation had taken into account the worst grid voltage conditions.
performed for lower grid voltages would be non-conservative. The team reviewed this
  Analysis: The team determined that a performance deficiency existed because the
item and determined that calculation C-EE-015.03-003 was superseded with calculation
  licensee failed to analyze the grid voltage under worst case design conditions. Since
C-EE-015.03-008, which utilized the ETAP program described in Section 4OA3(2)b.7.  
  there was a performance deficiency, the team compared this performance deficiency to
The new calculation had taken into account the worst grid voltage conditions.
  the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
Analysis: The team determined that a performance deficiency existed because the
  Reactor Inspection Reports." The team concluded that the issue was minor because
licensee failed to analyze the grid voltage under worst case design conditions. Since
  although the licensee had to perform calculations, the new calculation had taken into
there was a performance deficiency, the team compared this performance deficiency to
  account the worst grid voltage conditions and the results were acceptable.
the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
  Enforcement: The failure to translate the worst case grid voltage into calculations of
Reactor Inspection Reports." The team concluded that the issue was minor because
  record constituted a violation of 10 CFR Appendix B, Criterion III, which has minor
although the licensee had to perform calculations, the new calculation had taken into
  significance and is not subject to enforcement action in accordance with Section IV of
account the worst grid voltage conditions and the results were acceptable.
  the NRCs Enforcement Policy. The licensee entered the issue into its CAP as
Enforcement: The failure to translate the worst case grid voltage into calculations of
  CRs 02-06302 and 02-06837.
record constituted a violation of 10 CFR Appendix B, Criterion III, which has minor
  While minor violations are not normally documented in inspection reports, the team
significance and is not subject to enforcement action in accordance with Section IV of
  determined that documentation was appropriate in this case it represented an example
the NRCs Enforcement Policy. The licensee entered the issue into its CAP as
  of calculation weakness and the underlying cause is similar to that of other findings in
CRs 02-06302 and 02-06837.
  this report.
While minor violations are not normally documented in inspection reports, the team
                                            38                                      Enclosure
determined that documentation was appropriate in this case it represented an example
of calculation weakness and the underlying cause is similar to that of other findings in
this report.


(3)   Detailed Team Review of Licensee Corrective Actions Implemented to Address
Enclosure
      Mechanical Issues Previously Identified by NRC or the Licensee
39
a.   Inspection Scope
(3)
      The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,
Detailed Team Review of Licensee Corrective Actions Implemented to Address
      and resolve the identified equipment, human performance or programmatic adverse to
Mechanical Issues Previously Identified by NRC or the Licensee
      quality plant conditions. The team mainly focused on plant systems design and
  a.
      licensing basis requirements issues which were previously identified by the NRC, the
Inspection Scope
      licensee and others during various design reviews conducted in 2002. The team
The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,
      assessed effectiveness of the licensees corrective actions implemented to address
and resolve the identified equipment, human performance or programmatic adverse to
      previously identified mechanical engineering design issues.
quality plant conditions. The team mainly focused on plant systems design and
b.   Observations and Findings
licensing basis requirements issues which were previously identified by the NRC, the
  .1 High Pressure Injection Pump Operation Under Long Term Minimum Flow
licensee and others during various design reviews conducted in 2002. The team
      Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
assessed effectiveness of the licensees corrective actions implemented to address
      having very low safety significance (Green). Specifically, the licensee failed to verify
previously identified mechanical engineering design issues.
      that the HPI pumps could operate under design basis minimum flow requirements since
  b.
      initial plant startup. Following discovery that the design basis minimum flow
Observations and Findings
      requirements were significantly below industry standards, the licensee entered the issue
    .1
      into its corrective action program, performed a test which demonstrated satisfactory
High Pressure Injection Pump Operation Under Long Term Minimum Flow
      pump operation for an extended period of time at a higher flow rate, and began the
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
      steps to change the design basis minimum requirement. The primary cause of this
having very low safety significance (Green). Specifically, the licensee failed to verify
      violation was related to the cross-cutting area of corrective action because although this
that the HPI pumps could operate under design basis minimum flow requirements since
      issue was identified by the NRC in Information Notice (IN) 87-59, "Potential RHR Pump
initial plant startup. Following discovery that the design basis minimum flow
      Loss," in 1987 and in Bulletin 88-04, "Potential Safety-Related Pump Loss," in 1988, the
requirements were significantly below industry standards, the licensee entered the issue
      licensee failed to take action to correct it until it was specifically identified as applying to
into its corrective action program, performed a test which demonstrated satisfactory
      Davis Besse during the SSDI in 2002, and yet again during the CATI in 2003.
pump operation for an extended period of time at a higher flow rate, and began the
      Description: On November 17, 1987, the NRC issued an information notice describing
steps to change the design basis minimum requirement. The primary cause of this
      two concerns identified by a Nuclear Safety System Supply vendor which had the
violation was related to the cross-cutting area of corrective action because although this
      potential to impact safety operation of ECCS pumps. Specifically, IN 87-59 described
issue was identified by the NRC in Information Notice (IN) 87-59, "Potential RHR Pump
      two concerns, the second of which involved the adequacy of the minimum flow
Loss," in 1987 and in Bulletin 88-04, "Potential Safety-Related Pump Loss," in 1988, the
      recirculation line capacity even for single pump operation. The IN noted that the vendor
licensee failed to take action to correct it until it was specifically identified as applying to
      specifically stated that these concerns might also be applicable to high pressure safety
Davis Besse during the SSDI in 2002, and yet again during the CATI in 2003.
      injection pumps. On May 5, 1988, the NRC followed the IN with an NRC Bulletin
Description: On November 17, 1987, the NRC issued an information notice describing
      addressing the same concerns. Item 3 of the bulletin requested that licensees evaluate
two concerns identified by a Nuclear Safety System Supply vendor which had the
      the adequacy of the minimum flow bypass lines for safety-related centrifugal pumps with
potential to impact safety operation of ECCS pumps. Specifically, IN 87-59 described
      respect to damage resulting from operation and testing in the minimum flow mode. It
two concerns, the second of which involved the adequacy of the minimum flow
      stated that the evaluation should include consideration of both the effects of cumulative
recirculation line capacity even for single pump operation. The IN noted that the vendor
      operating hours in the minimum flow mode over the lifetime of the plant and during the
specifically stated that these concerns might also be applicable to high pressure safety
      postulated accident scenario involving the largest time spent in the minimum
injection pumps. On May 5, 1988, the NRC followed the IN with an NRC Bulletin
      recirculation flow mode. It also requested that the evaluation include verification from the
addressing the same concerns. Item 3 of the bulletin requested that licensees evaluate
      pump suppliers that current minimum flow rates were sufficient to ensure that there will
the adequacy of the minimum flow bypass lines for safety-related centrifugal pumps with
      be no pump damage from low flow operation.
respect to damage resulting from operation and testing in the minimum flow mode. It
                                                39                                          Enclosure
stated that the evaluation should include consideration of both the effects of cumulative
operating hours in the minimum flow mode over the lifetime of the plant and during the
postulated accident scenario involving the largest time spent in the minimum
recirculation flow mode. It also requested that the evaluation include verification from the
pump suppliers that current minimum flow rates were sufficient to ensure that there will
be no pump damage from low flow operation.


During the SSDI, the NRC reviewed the HPI pump minimum flow capacity and raised
Enclosure
two concerns related minimum flow and no flow conditions. The NRC determined that
40
During the SSDI, the NRC reviewed the HPI pump minimum flow capacity and raised  
two concerns related minimum flow and no flow conditions. The NRC determined that
the adequacy of the minimum recirculation flow value of 35 gallons per minute (gpm)
the adequacy of the minimum recirculation flow value of 35 gallons per minute (gpm)
was questionable and that there was a potentially unanalyzed condition during a small
was questionable and that there was a potentially unanalyzed condition during a small
break loss of coolant accident (LOCA). For certain small break LOCAs, the NRC
break loss of coolant accident (LOCA). For certain small break LOCAs, the NRC
determined that the HPI pumps potentially could be required to operate under conditions
determined that the HPI pumps potentially could be required to operate under conditions
where the reactor coolant system (RCS) pressure would be very close to or possibly
where the reactor coolant system (RCS) pressure would be very close to or possibly
greater than the pressure under which the HPI pumps could inject. During the
greater than the pressure under which the HPI pumps could inject. During the
recirculation phase, after the contents of the borated water storage tank (BWST) were
recirculation phase, after the contents of the borated water storage tank (BWST) were
injected, the return line to the BWST was procedurally required to be manually isolated
injected, the return line to the BWST was procedurally required to be manually isolated
from the control room to prevent an unmonitored release of radiation. The HPI pumps
from the control room to prevent an unmonitored release of radiation. The HPI pumps
had a defined mission time of 30 days (720 hours) where the pumps were required to
had a defined mission time of 30 days (720 hours) where the pumps were required to
remain operable. The licensee issued CRs 02-07684 (for the adequacy of the 35 gpm)
remain operable. The licensee issued CRs 02-07684 (for the adequacy of the 35 gpm)
and 02-06702 (on the potentially unanalyzed lack of flow condition) to evaluate these
and 02-06702 (on the potentially unanalyzed lack of flow condition) to evaluate these
concerns.
concerns.  
The licensee resolved the issue of not having a minimum flow recirculation path during
The licensee resolved the issue of not having a minimum flow recirculation path during
the sump recirculation phase by implementing a modification to provide a new minimum
the sump recirculation phase by implementing a modification to provide a new minimum
recirculation flow path for the HPI pumps via a connection through the decay heat
recirculation flow path for the HPI pumps via a connection through the decay heat
removal (DHR) injection line. This modification was designed to the same 35 gpm flow
removal (DHR) injection line. This modification was designed to the same 35 gpm flow
rate as the original recirculation line because, in evaluating CR 02-07684, the licensee
rate as the original recirculation line because, in evaluating CR 02-07684, the licensee
concluded that the 35 gpm was adequate. During the 2003 CATI, the team again
concluded that the 35 gpm was adequate. During the 2003 CATI, the team again
questioned the adequacy of the 35 gpm minimum flow, especially in light of the 1988
questioned the adequacy of the 35 gpm minimum flow, especially in light of the 1988
Bulletin. Although the licensee had not reviewed the Bulletin response as part of their
Bulletin. Although the licensee had not reviewed the Bulletin response as part of their
evaluation of CR 02-07684, they resurrected the document in response to team
evaluation of CR 02-07684, they resurrected the document in response to team
questions. The team determined that the licensees response to the Bulletin was based
questions. The team determined that the licensees response to the Bulletin was based
on the results from three 10-minute vibration runs; these tests showed no appreciable
on the results from three 10-minute vibration runs; these tests showed no appreciable
increase in vibration. The licensee also had contacted the pump vendor, who was
increase in vibration. The licensee also had contacted the pump vendor, who was
unable to confirm that the 35 gpm flow was adequate to ensure that HPI pumps would
unable to confirm that the 35 gpm flow was adequate to ensure that HPI pumps would
not experience degradation as a result of hydraulic instability or impeller recirculation.
not experience degradation as a result of hydraulic instability or impeller recirculation.  
The team noted that industry experience indicated that long term pump minimum flow
The team noted that industry experience indicated that long term pump minimum flow
value should be close to 25 percent of flow at the pumps best efficiency point. For the
value should be close to 25 percent of flow at the pumps best efficiency point. For the
HPI pumps, the flow at the best efficiency point was 600 gpm, which would indicate that
HPI pumps, the flow at the best efficiency point was 600 gpm, which would indicate that
a minimum flow on the order of 150 gpm would be appropriate as compared to the 35
a minimum flow on the order of 150 gpm would be appropriate as compared to the 35
gpm which was in the licensee's design specification at the time of the inspection.
gpm which was in the licensee's design specification at the time of the inspection.
In response to the team again raising the issue on the adequacy of the HPI pump
In response to the team again raising the issue on the adequacy of the HPI pump
minimum flow value of 35 gpm, the licensee wrote CRs 03-06526 and 03-06519. As
minimum flow value of 35 gpm, the licensee wrote CRs 03-06526 and 03-06519. As
part of the investigation summary in CR 03-06526, the licensee provided evaluations by
part of the investigation summary in CR 03-06526, the licensee provided evaluations by
three pump experts. These evaluations appeared to only justify continued operation
three pump experts. These evaluations appeared to only justify continued operation
based on the effects of cumulative operating hours in the minimum flow mode over the
based on the effects of cumulative operating hours in the minimum flow mode over the
experienced lifetime of the plant. The team was unable to find any evaluation of the
experienced lifetime of the plant. The team was unable to find any evaluation of the
ability of the HPI pumps to function on minimum flow during the licensee's stated
ability of the HPI pumps to function on minimum flow during the licensee's stated
mission time of 30 days; this included any evaluation by the licensee that a shorter
mission time of 30 days; this included any evaluation by the licensee that a shorter
mission time was appropriate for operating entirely on minimum flow. The team noted
mission time was appropriate for operating entirely on minimum flow. The team noted
that this issue was assigned a priority of "CF" which meant that the licensee did not
that this issue was assigned a priority of "CF" which meant that the licensee did not
believe that any cause evaluation was required, just that the issue had to be resolved.
believe that any cause evaluation was required, just that the issue had to be resolved.  
The licensee's basis for designating the CR as a "CF" was that the pump only had to
The licensee's basis for designating the CR as a "CF" was that the pump only had to
operate "occasionally" in the minimum flow configuration - which did not recognize the
operate "occasionally" in the minimum flow configuration - which did not recognize the
                                          40                                    Enclosure


pumps safety function. At the end of the on-site inspection, the licensee was still
Enclosure
41
pumps safety function. At the end of the on-site inspection, the licensee was still
evaluating the issue.
evaluating the issue.
In December 2003, the team performed a limited review of the licensees evaluation of a
In December 2003, the team performed a limited review of the licensees evaluation of a
test performed on one of the HPI pumps. This test was run for 6 hours at a flow of 53
test performed on one of the HPI pumps. This test was run for 6 hours at a flow of 53
gpm. The basis for establishing a test duration of 6 hours appeared to be that the pump
gpm. The basis for establishing a test duration of 6 hours appeared to be that the pump
shaft would experience a million cycles of operation and that, if pump failure was going
shaft would experience a million cycles of operation and that, if pump failure was going
to occur, it should occur within that time period. However, the licensee did not either
to occur, it should occur within that time period. However, the licensee did not either
extrapolate the number of cycles to the stated mission time of 30 days nor did they
extrapolate the number of cycles to the stated mission time of 30 days nor did they
provide any basis statement as to why 6 hours would be the maximum time that the
provide any basis statement as to why 6 hours would be the maximum time that the
pump would spend on minimum flow. The basis for establishing the flow of 53 gpm was
pump would spend on minimum flow. The basis for establishing the flow of 53 gpm was
that it was the actual flow through the installed orifice. However, the licensee did not
that it was the actual flow through the installed orifice. However, the licensee did not
extrapolate the flow back to the design basis minimum or take steps to change the
extrapolate the flow back to the design basis minimum or take steps to change the
design basis. While it was highly unlikely that the pump would experience flows below
design basis. While it was highly unlikely that the pump would experience flows below
the 53 gpm for the current orifice, the team noted that this test was run on only one of
the 53 gpm for the current orifice, the team noted that this test was run on only one of
four recirculation lines (including the two new ones installed during the 13th refueling
four recirculation lines (including the two new ones installed during the 13th refueling
outage). The team noted that the newly installed lines had throttle valves which could
outage). The team noted that the newly installed lines had throttle valves which could
be adjusted to a flow rate anywhere in the acceptance criteria band, including a value
be adjusted to a flow rate anywhere in the acceptance criteria band, including a value
well below the demonstrated flow rate. The team also noted that the surveillance test
well below the demonstrated flow rate. The team also noted that the surveillance test
data for the 1-2 HPI pump (the one not tested) showed the recirculation flow rates on
data for the 1-2 HPI pump (the one not tested) showed the recirculation flow rates on
this pump were closer to the high end of the acceptance criteria band where the
this pump were closer to the high end of the acceptance criteria band where the
licensee was supposed to evaluate replacement of the orifice.
licensee was supposed to evaluate replacement of the orifice.  
As a result of the teams questions, on February 8, 2004, the licensee provided an
As a result of the teams questions, on February 8, 2004, the licensee provided an
operability determination which addressed pump operability under the design conditions.
operability determination which addressed pump operability under the design conditions.
The licensee concluded that the HPI pumps are capable of providing the necessary flow
The licensee concluded that the HPI pumps are capable of providing the necessary flow
over the mission time of 30 days with extended periods at minimum recirculation flow.
over the mission time of 30 days with extended periods at minimum recirculation flow.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to demonstrate that the pump could successfully perform its safety
licensee failed to demonstrate that the pump could successfully perform its safety
function for the stated mission time of 30 days and under the initial design minimum flow
function for the stated mission time of 30 days and under the initial design minimum flow
rate of 35 gpm by either test or evaluation prior to 2004. Since there was a performance
rate of 35 gpm by either test or evaluation prior to 2004. Since there was a performance
deficiency, the team compared this performance deficiency to the minor questions
deficiency, the team compared this performance deficiency to the minor questions
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
Reports." The team concluded that the issue was more than minor because the
Reports." The team concluded that the issue was more than minor because the
licensee had to perform a test to demonstrate that design basis requirements could be
licensee had to perform a test to demonstrate that design basis requirements could be
met and because the test results determined that the design basis requirements needed
met and because the test results determined that the design basis requirements needed
to be changed to ensure that the HPI pumps could perform their accident required
to be changed to ensure that the HPI pumps could perform their accident required
function. This was an issue which affected the mitigating systems cornerstone. The
function. This was an issue which affected the mitigating systems cornerstone. The
team reviewed this finding in accordance with IMC 0609, "Significance Determination
team reviewed this finding in accordance with IMC 0609, "Significance Determination
Process. Although the pumps had not been tested at the minimum design flow valve,
Process. Although the pumps had not been tested at the minimum design flow valve,
the team was unable to conclude that the safety function of the pumps had actually
the team was unable to conclude that the safety function of the pumps had actually
been lost. This was based on a review of surveillance test results from June 2001
been lost. This was based on a review of surveillance test results from June 2001
through December 2003. These test results showed the lowest flow rate for either pump
through December 2003. These test results showed the lowest flow rate for either pump
to be 49 gpm. Although this was slightly outside the licensee's new operability band, the
to be 49 gpm. Although this was slightly outside the licensee's new operability band, the
team deemed it likely that the pumps would have performed had they been called upon.
team deemed it likely that the pumps would have performed had they been called upon.  
Therefore, the team answered no to all five screening questions in the Phase 1
Therefore, the team answered no to all five screening questions in the Phase 1
Screening Worksheet under the Mitigating Systems column. The team concluded the
Screening Worksheet under the Mitigating Systems column. The team concluded the
issue was of very low safety significance (Green).
issue was of very low safety significance (Green).
                                          41                                      Enclosure


  The performance deficiency of not having any recirculation lines once the BWST
Enclosure
  emptied is addressed in Section 4OA3(6)b.3.
42
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
The performance deficiency of not having any recirculation lines once the BWST
  measures be established to assure that applicable regulatory requirements and the
emptied is addressed in Section 4OA3(6)b.3.
  design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
  instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
  checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
  use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
  testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
  Contrary to the above, the licensee failed to verify the adequacy of the design of the
use of alternate or simplified calculational methods, or by the performance of a suitable
  minimum recirculation line flow rate of 35 gpm. Specifically, on December 23, 2003, the
testing program.
  licensee determined that the minimum flow rate of 35 gpm could not be verified and the
Contrary to the above, the licensee failed to verify the adequacy of the design of the
  minimum value which had been verified by a suitable testing program was 53 gpm.
minimum recirculation line flow rate of 35 gpm. Specifically, on December 23, 2003, the
  Because this violation was of very low safety significance and because it was entered
licensee determined that the minimum flow rate of 35 gpm could not be verified and the
  into the licensees CAP as CRs 03-11268, 03-11431 and 04-01050, this violation is
minimum value which had been verified by a suitable testing program was 53 gpm.  
  being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy.
Because this violation was of very low safety significance and because it was entered
  (NCV 05000346/2003010-08)
into the licensees CAP as CRs 03-11268, 03-11431 and 04-01050, this violation is
.2 Increased Dose Consequences Due to Degraded Thermal Performance
being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy.  
  Operation of Degraded Containment Air Coolers
(NCV 05000346/2003010-08)
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    .2
  having very low safety significance. Specifically, the licensee failed to assess an
Increased Dose Consequences Due to Degraded Thermal Performance
  increase in the offsite dose to the public following a postulated design basis accident
Operation of Degraded Containment Air Coolers
  due to increased containment pressure. Following discovery, the licensee entered the
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  issue into its corrective action process and performed the necessary analysis. The
having very low safety significance. Specifically, the licensee failed to assess an
  primary cause of this violation was related to the cross-cutting area of problem
increase in the offsite dose to the public following a postulated design basis accident
  identification and resolution, because, although the issue had been previously identified,
due to increased containment pressure. Following discovery, the licensee entered the
  the licensee had failed to identify that a revised dose assessment was needed until
issue into its corrective action process and performed the necessary analysis. The
  prompted by the NRC.
primary cause of this violation was related to the cross-cutting area of problem
  Description: In 2002, the licensee identified that the CACs were significantly degraded
identification and resolution, because, although the issue had been previously identified,
  and required replacement. In December 2002, the licensee issued LER
the licensee had failed to identify that a revised dose assessment was needed until
  05000346/2002-008-00, which discussed the degradation. During the review of
prompted by the NRC.
  CR 03-00120 and LER 05000346/2002-008-00 and -01, the team noted that the issue of
Description: In 2002, the licensee identified that the CACs were significantly degraded
  potentially increased offsite doses due to the degraded CACs was not addressed with a
and required replacement. In December 2002, the licensee issued LER
  technical basis in the evaluation of CR 03-00120. In particular, the time to reach half
05000346/2002-008-00, which discussed the degradation. During the review of
  containment design pressure after a design basis LOCA increased from 16.7 hours to
CR 03-00120 and LER 05000346/2002-008-00 and -01, the team noted that the issue of
  58.3 hours because of degraded CAC performance. The specified acceptance criteria
potentially increased offsite doses due to the degraded CACs was not addressed with a
  was that the containment pressure be reduced to 50 percent of the containment design
technical basis in the evaluation of CR 03-00120. In particular, the time to reach half
  pressure within 24 hours as recommended by Regulatory Guide 1.4, "Assumptions
containment design pressure after a design basis LOCA increased from 16.7 hours to
  Used for Evaluating the Potential Radiological Consequences of a Loss of Coolant
58.3 hours because of degraded CAC performance. The specified acceptance criteria
  Accident for Pressurized Water Reactors." The analyses performed for the degraded
was that the containment pressure be reduced to 50 percent of the containment design
  CAC operability assessment did not meet this requirement. However, the licensee
pressure within 24 hours as recommended by Regulatory Guide 1.4, "Assumptions
  concluded in CR 03-00120 that exceeding the half containment design pressure rating
Used for Evaluating the Potential Radiological Consequences of a Loss of Coolant
  within 24 hours had no impact on dose consequences analyzed in accordance with
Accident for Pressurized Water Reactors." The analyses performed for the degraded
  Regulatory Guide 1.4 assumptions, without documenting any basis for the statement.
CAC operability assessment did not meet this requirement. However, the licensee
                                            42                                    Enclosure
concluded in CR 03-00120 that exceeding the half containment design pressure rating
within 24 hours had no impact on dose consequences analyzed in accordance with
Regulatory Guide 1.4 assumptions, without documenting any basis for the statement.


Enclosure
43
When first questioned by the team, the licensee acknowledged that there was no formal
When first questioned by the team, the licensee acknowledged that there was no formal
dose assessment to support the conclusion documented in CR 03-00120. The licensee
dose assessment to support the conclusion documented in CR 03-00120. The licensee
then performed a calculation which indicated that, although the offsite radiological doses
then performed a calculation which indicated that, although the offsite radiological doses
increased, they were still less than the Regulatory Guide 1.4 allowables when
increased, they were still less than the Regulatory Guide 1.4 allowables when
accounting for the increase in containment pressure. The team did not review this
accounting for the increase in containment pressure. The team did not review this
calculation.
calculation.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to verify that increased containment pressure due to degraded CAC
licensee failed to verify that increased containment pressure due to degraded CAC
performance would not result in unacceptable offsite dose consequences. Since there
performance would not result in unacceptable offsite dose consequences. Since there
was a performance deficiency, the team compared this performance deficiency to the
was a performance deficiency, the team compared this performance deficiency to the
minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
Reactor Inspection Reports." The team concluded that the issue was more than minor
Reactor Inspection Reports." The team concluded that the issue was more than minor
because the licensee had to perform calculations to show that the increased time at
because the licensee had to perform calculations to show that the increased time at
higher containment pressures did not result in doses being above regulatory guide
higher containment pressures did not result in doses being above regulatory guide
allowables. The team reviewed this finding in accordance with IMC 0609, "Significance
allowables. The team reviewed this finding in accordance with IMC 0609, "Significance
Determination Process.
Determination Process.
The team reviewed the SDP questions for reactor safety, occupation radiation safety
The team reviewed the SDP questions for reactor safety, occupation radiation safety
and public radiation safety contained in MC 0612, Appendix B, Issue Screening. The
and public radiation safety contained in MC 0612, Appendix B, Issue Screening. The
team assessed the finding through Phase 1 of the SDP. According to the Davis-Besse
team assessed the finding through Phase 1 of the SDP. According to the Davis-Besse
Risk-informed Inspection Notebook, the CACs had both a barrier integrity and mitigating
Risk-informed Inspection Notebook, the CACs had both a barrier integrity and mitigating
system cornerstone function. However, the team determined that the issue was not
system cornerstone function. However, the team determined that the issue was not
covered by any of the revised oversight cornerstones and was not suitable for SDP
covered by any of the revised oversight cornerstones and was not suitable for SDP
analysis since the finding pertained to offsite dose calculations rather than CAC
analysis since the finding pertained to offsite dose calculations rather than CAC
performance. Therefore, this finding was reviewed by Regional Management, in
performance. Therefore, this finding was reviewed by Regional Management, in
accordance with IMC 0612. The finding was determined to be of very low safety
accordance with IMC 0612. The finding was determined to be of very low safety
significance (Green) because the issue regarded increased containment pressure,
significance (Green) because the issue regarded increased containment pressure,
related to offsite dose consequences, and although the offsite radiological doses
related to offsite dose consequences, and although the offsite radiological doses
increased, the values were still less than the Regulatory Guide 1.4 allowables.
increased, the values were still less than the Regulatory Guide 1.4 allowables.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
measures be established to assure that applicable regulatory requirements and the
measures be established to assure that applicable regulatory requirements and the
design basis were correctly translated into specifications, drawings, procedures, and
design basis were correctly translated into specifications, drawings, procedures, and
instructions. Furthermore, it requires that measures be provided for verifying or
instructions. Furthermore, it requires that measures be provided for verifying or
checking the adequacy of design, such as by the performance of design reviews, by the
checking the adequacy of design, such as by the performance of design reviews, by the
use of alternate or simplified calculational methods, or by the performance of a suitable
use of alternate or simplified calculational methods, or by the performance of a suitable
testing program.
testing program.
Contrary to the above, the licensee failed to implement design control measures to
Contrary to the above, the licensee failed to implement design control measures to
verify the adequacy of design basis calculations. Specifically, the licensee failed to
verify the adequacy of design basis calculations. Specifically, the licensee failed to
demonstrate that increased containment pressure due to degraded CAC performance
demonstrate that increased containment pressure due to degraded CAC performance
did not result in unacceptable offsite dose consequences. The licensee entered this
did not result in unacceptable offsite dose consequences. The licensee entered this
issue into its CAP as CR 03-03980. Because this violation was of very low safety
issue into its CAP as CR 03-03980. Because this violation was of very low safety
significance and because it was entered into the licensees CAP, this violation is being
significance and because it was entered into the licensees CAP, this violation is being
treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy. (NCV
treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy. (NCV
05000346/2003010-09)
05000346/2003010-09)
                                          43                                      Enclosure


.3 Containment Air Cooler Air Flow Calculation Concerns
Enclosure
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
44
  having very low safety significance (Green). Specifically, the licensee failed to correctly
    .3
  identify and translate the design basis requirements into the CACs airflow analyses and
Containment Air Cooler Air Flow Calculation Concerns
  motor horsepower sizing calculations. Following discovery, the licensee entered the
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  issue into its corrective action program and performed a new analysis for the motor.
having very low safety significance (Green). Specifically, the licensee failed to correctly
  The primary cause of this violation was related to the cross-cutting area of problem
identify and translate the design basis requirements into the CACs airflow analyses and
  identification and resolution as the licensee had previously identified issues with the
motor horsepower sizing calculations. Following discovery, the licensee entered the
  motors, but had not reviewed the design calculation of record.
issue into its corrective action program and performed a new analysis for the motor.  
  Description: During review of CR 03-00120, which was the licensees collective
The primary cause of this violation was related to the cross-cutting area of problem
  significance review in regard to the degraded condition of the CACs, the team also
identification and resolution as the licensee had previously identified issues with the
  reviewed calculation 28.003. This calculation was used to size the existing CAC motor.
motors, but had not reviewed the design calculation of record.
  The team determined that the calculation was performed in 1970 and applied design
Description: During review of CR 03-00120, which was the licensees collective
  information from the Oconee Nuclear Power Plant to Davis-Besse without correction for
significance review in regard to the degraded condition of the CACs, the team also
  actual Davis-Besse conditions. The NRC team questioned the design values for system
reviewed calculation 28.003. This calculation was used to size the existing CAC motor.  
  resistance, airflow, and density used in the calculation for sizing CAC motors since there
The team determined that the calculation was performed in 1970 and applied design
  was no reference to Davis-Besse equipment or systems.
information from the Oconee Nuclear Power Plant to Davis-Besse without correction for
  Calculation 28.003 specified a requirement for a 45 horsepower motor, whereas at
actual Davis-Besse conditions. The NRC team questioned the design values for system
  Davis-Besse, a 40 horsepower motor was actually installed. In addition, the density
resistance, airflow, and density used in the calculation for sizing CAC motors since there
  used in calculation 28.003 was different than that used for the postulated breaks
was no reference to Davis-Besse equipment or systems.
  analyzed in calculation C-NSA-060.05-010. For example, C-NSA-060.05-010, the
Calculation 28.003 specified a requirement for a 45 horsepower motor, whereas at
  computed density profile remained at or below 0.132 pounds per cubic foot (lb/ft3) for
Davis-Besse, a 40 horsepower motor was actually installed. In addition, the density
  the first 6 seconds, increased to 0.152 lb/ft3 from 7 to 16 seconds, then dropped to
used in calculation 28.003 was different than that used for the postulated breaks
  0.132 lb/ft3 at approximately 250 seconds. In contrast, calculation 28.003 used the less
analyzed in calculation C-NSA-060.05-010. For example, C-NSA-060.05-010, the
  conservative density profile of 0.132 lb/ft3 throughout. Following the teams questioning,
computed density profile remained at or below 0.132 pounds per cubic foot (lb/ft3) for
  the licensee performed a new calculation which showed that the CAC motors were
the first 6 seconds, increased to 0.152 lb/ft3 from 7 to 16 seconds, then dropped to
  appropriately sized.
0.132 lb/ft3 at approximately 250 seconds. In contrast, calculation 28.003 used the less
  The team also noted that the vendor who supplied the CAC motors had submitted a
conservative density profile of 0.132 lb/ft3 throughout. Following the teams questioning,
  Part 21 notice to the licensee in May 2002. According to LER 05000346/2002-008, this
the licensee performed a new calculation which showed that the CAC motors were
  issue was entered into the CAP but was determined to not be of significance due to the
appropriately sized.
  CAC motors being refurbished as part of the overall CAC refurbishment. The team
The team also noted that the vendor who supplied the CAC motors had submitted a
  considered this to be an example of poor engineering response to an issue specifically,
Part 21 notice to the licensee in May 2002. According to LER 05000346/2002-008, this
  the licensee had determined that the CAC motors needed to be refurbished, but had
issue was entered into the CAP but was determined to not be of significance due to the
  either not looked at the design basis calculation for the motors prior to beginning the
CAC motors being refurbished as part of the overall CAC refurbishment. The team
  refurbishment, or had not performed an adequate review.
considered this to be an example of poor engineering response to an issue specifically,  
  Analysis: The team determined that a performance deficiency existed because the
the licensee had determined that the CAC motors needed to be refurbished, but had
  licensee failed to analyze CAC fan sizing with respect to actual airflow, air density,
either not looked at the design basis calculation for the motors prior to beginning the
  pressure drop, and motor size. Since there was a performance deficiency, the team
refurbishment, or had not performed an adequate review.
  compared this performance deficiency to the minor questions contained in Appendix B,
Analysis: The team determined that a performance deficiency existed because the
  "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
licensee failed to analyze CAC fan sizing with respect to actual airflow, air density,
  concluded that the issue was more than minor because the licensee had to revise the
pressure drop, and motor size. Since there was a performance deficiency, the team
  associated calculation to evaluate the existing motor to ensure the CACs would be able
compared this performance deficiency to the minor questions contained in Appendix B,
  to perform their design function. The team assessed the finding through Phase 1 of the
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
  SDP. According to the Davis-Besse Risk-informed Inspection Notebook, the CACs had
concluded that the issue was more than minor because the licensee had to revise the
  both a barrier integrity and mitigating system function. The team determined that this
associated calculation to evaluate the existing motor to ensure the CACs would be able
                                            44                                      Enclosure
to perform their design function. The team assessed the finding through Phase 1 of the
SDP. According to the Davis-Besse Risk-informed Inspection Notebook, the CACs had
both a barrier integrity and mitigating system function. The team determined that this


  issue affected both functions. Because the issue involved both the mitigating system
Enclosure
  and barrier integrity cornerstones, the team entered Phase 2 of the reactor safety SDP.
45
  The team completed the Phase 2 worksheets for the following scenarios: Transients,
issue affected both functions. Because the issue involved both the mitigating system
  Transients with Loss of the Power Conversion System, Small LOCA, Loss of Offsite
and barrier integrity cornerstones, the team entered Phase 2 of the reactor safety SDP.
  Power (LOOP), Steam Generator (SG) Tube Rupture (SGTR), Main Steam Line Break
The team completed the Phase 2 worksheets for the following scenarios: Transients,
  (MSLB), Loss of Instrument Air, Loss of a 4 kilovolt (kV) Bus, Loss of DC Buses D1P
Transients with Loss of the Power Conversion System, Small LOCA, Loss of Offsite
  and D2P and Loss of One Emergency AC Train. Completion of these worksheets
Power (LOOP), Steam Generator (SG) Tube Rupture (SGTR), Main Steam Line Break
  resulted in two sequences rated as "12", three sequences rated as "11", four sequences
(MSLB), Loss of Instrument Air, Loss of a 4 kilovolt (kV) Bus, Loss of DC Buses D1P
  rated as "10", two sequences rated as "9", and three sequences rated as "8". This
and D2P and Loss of One Emergency AC Train. Completion of these worksheets
  information was entered into the "Counting Rule Worksheet" and a final evaluation was
resulted in two sequences rated as "12", three sequences rated as "11", four sequences
  obtained that the issue was of very low safety significance (Green).
rated as "10", two sequences rated as "9", and three sequences rated as "8". This
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
information was entered into the "Counting Rule Worksheet" and a final evaluation was
  measures be established to assure that applicable regulatory requirements and the
obtained that the issue was of very low safety significance (Green).
  design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
  instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
  checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
  use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
  testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
  Contrary to this requirement, the licensee failed to correctly translate the design basis
use of alternate or simplified calculational methods, or by the performance of a suitable
  into specifications, drawing, procedures, and instructions. Specifically, the licensee
testing program.
  failed to correctly identify and translate the design basis requirements such as actual
Contrary to this requirement, the licensee failed to correctly translate the design basis
  airflow, air density, pressure drop, and motor size, into the CAC airflow analyses and
into specifications, drawing, procedures, and instructions. Specifically, the licensee
  motor horsepower sizing calculations that demonstrated the ability of the safety-related
failed to correctly identify and translate the design basis requirements such as actual
  CACs to deliver the required design basis air flow rate to the containment during an
airflow, air density, pressure drop, and motor size, into the CAC airflow analyses and
  accident. The licensee entered this issue into its CAP as CR 03-07009. Because this
motor horsepower sizing calculations that demonstrated the ability of the safety-related
  violation was of very low safety significance and because it was entered into the
CACs to deliver the required design basis air flow rate to the containment during an
  licensees CAP, this violation is being treated as an NCV consistent with Section VI.A of
accident. The licensee entered this issue into its CAP as CR 03-07009. Because this
  the NRC Enforcement Policy. (NCV 05000346/2003010-10)
violation was of very low safety significance and because it was entered into the
.4 Accumulator Sizing Calculation Errors
licensees CAP, this violation is being treated as an NCV consistent with Section VI.A of
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
the NRC Enforcement Policy. (NCV 05000346/2003010-10)
  having very low safety significance (Green). Specifically, the licensee failed to
    .4
  implement effective design control measures to check and verify the adequacy of the
Accumulator Sizing Calculation Errors
  design basis calculation performed for sizing the new accumulators used to hold the SW
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  containment isolation valves closed on a loss of instrument air. Following discovery, the
having very low safety significance (Green). Specifically, the licensee failed to
  licensee entered the issue into its corrective action program, revised the calculations,
implement effective design control measures to check and verify the adequacy of the
  and changed the accumulator medium from compressed air to nitrogen.
design basis calculation performed for sizing the new accumulators used to hold the SW
  Description: In 2002, SSDI team identified a NCV for failing to correctly translate the
containment isolation valves closed on a loss of instrument air. Following discovery, the
  design basis requirements for sizing of the safety-related backup air supplies for
licensee entered the issue into its corrective action program, revised the calculations,
  containment isolation valves SW-1356, SW-1357, and SW-1358 into the design. The
and changed the accumulator medium from compressed air to nitrogen.
  licensees corrective action was to install new accumulators sized to hold the valves
Description: In 2002, SSDI team identified a NCV for failing to correctly translate the
  closed. The team reviewed several revisions of calculation C-ME-011.06-007 which
design basis requirements for sizing of the safety-related backup air supplies for
  sized the new accumulators.
containment isolation valves SW-1356, SW-1357, and SW-1358 into the design. The
                                              45                                    Enclosure
licensees corrective action was to install new accumulators sized to hold the valves
closed. The team reviewed several revisions of calculation C-ME-011.06-007 which
sized the new accumulators.


Enclosure
46
The team identified numerous errors in the calculation which required the calculation to
The team identified numerous errors in the calculation which required the calculation to
be revised. For example, in Revisions 0 and 1 of the calculation, the new accumulators
be revised. For example, in Revisions 0 and 1 of the calculation, the new accumulators
were intended to be filled with air as the licensee thought the valves only had to remain
were intended to be filled with air as the licensee thought the valves only had to remain
closed for 30 minutes. The licensee initially did not appear to recognize that the valves
closed for 30 minutes. The licensee initially did not appear to recognize that the valves
had a containment isolation design function which required the valves to remain closed
had a containment isolation design function which required the valves to remain closed
for 30 days until questioned by the team during the inspection. Following the teams
for 30 days until questioned by the team during the inspection. Following the teams
questions, the licensee changed the design to require that the new accumulators be
questions, the licensee changed the design to require that the new accumulators be
filled with nitrogen rather than air. In the last revision reviewed, the calculation
filled with nitrogen rather than air. In the last revision reviewed, the calculation
erroneously used the ideal gas law equations when sizing the nitrogen bottles without
erroneously used the ideal gas law equations when sizing the nitrogen bottles without
consideration of the compressibility of nitrogen at a pressure of 2000 pounds per square
consideration of the compressibility of nitrogen at a pressure of 2000 pounds per square
inch (psig). The calculation also indicated that the valve actuators were double acting
inch (psig). The calculation also indicated that the valve actuators were double acting
when other documents indicated that actuators were single acting. Additionally, the
when other documents indicated that actuators were single acting. Additionally, the
calculation could not stand alone without recourse to the author because certain
calculation could not stand alone without recourse to the author because certain
calculation steps were missing. The licensee revised the calculation to correct the
calculation steps were missing. The licensee revised the calculation to correct the
errors identified by the team. The team noted that the licensee was addressing past
errors identified by the team. The team noted that the licensee was addressing past
operability of the accumulators separately as part of LER 05000346/2003-001. This
operability of the accumulators separately as part of LER 05000346/2003-001. This
LER will be addressed in a separate IR.
LER will be addressed in a separate IR.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to verify the adequacy of the design basis calculation performed for
licensee failed to verify the adequacy of the design basis calculation performed for
sizing the accumulators prior to approving the calculation. Since there was a
sizing the accumulators prior to approving the calculation. Since there was a
performance deficiency, the team compared this performance deficiency to the minor
performance deficiency, the team compared this performance deficiency to the minor
questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
Inspection Reports." The team concluded that the issue was more than minor because
Inspection Reports." The team concluded that the issue was more than minor because
the licensee had to re-perform calculations and had to change the modification design
the licensee had to re-perform calculations and had to change the modification design
from having accumulators containing pressurized air to accumulators containing
from having accumulators containing pressurized air to accumulators containing
pressurized nitrogen. The team reviewed this finding in accordance with IMC 0609,
pressurized nitrogen. The team reviewed this finding in accordance with IMC 0609,
"Significance Determination Process.
"Significance Determination Process.
The team reviewed the SDP questions for reactor safety, occupation radiation safety
The team reviewed the SDP questions for reactor safety, occupation radiation safety
and public radiation safety contained in MC 0612, Appendix B, Issue Screening. The
and public radiation safety contained in MC 0612, Appendix B, Issue Screening. The
team assessed the finding through Phase 1 of the SDP. However, the team determined
team assessed the finding through Phase 1 of the SDP. However, the team determined
that the issue was not covered by any of the revised oversight cornerstones and was,
that the issue was not covered by any of the revised oversight cornerstones and was,
therefore, not suitable for SDP analysis. This determination was based on the issue
therefore, not suitable for SDP analysis. This determination was based on the issue
affecting containment isolation valves which provide a barrier to breach of containment
affecting containment isolation valves which provide a barrier to breach of containment
and potential offsite dose consequences. Therefore, this finding was reviewed by
and potential offsite dose consequences. Therefore, this finding was reviewed by
Regional Management, in accordance with IMC 0612. The finding was determined to be
Regional Management, in accordance with IMC 0612. The finding was determined to be
of very low safety significance (Green) because the issue regarded increased
of very low safety significance (Green) because the issue regarded increased
containment pressure and related to offsite dose consequences.
containment pressure and related to offsite dose consequences.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
measures be established to assure that applicable regulatory requirements and the
measures be established to assure that applicable regulatory requirements and the
design basis were correctly translated into specifications, drawings, procedures, and
design basis were correctly translated into specifications, drawings, procedures, and
instructions. Furthermore, it requires that measures be provided for verifying or
instructions. Furthermore, it requires that measures be provided for verifying or
checking the adequacy of design, such as by the performance of design reviews, by the
checking the adequacy of design, such as by the performance of design reviews, by the
use of alternate or simplified calculational methods, or by the performance of a suitable
use of alternate or simplified calculational methods, or by the performance of a suitable
testing program.
testing program.
                                          46                                        Enclosure


  Contrary to the above, the licensee failed to implement design control measures to
Enclosure
  check and verify the adequacy of the design basis calculation performed for sizing the
47
  accumulators used to hold containment isolation valves closed on a loss of instrument
Contrary to the above, the licensee failed to implement design control measures to
  air. The licensee entered the issue into its CAP as CR 03-06556. Because this violation
check and verify the adequacy of the design basis calculation performed for sizing the
  was of very low safety significance and because it was entered into the licensees CAP,
accumulators used to hold containment isolation valves closed on a loss of instrument
  this violation is being treated as an NCV consistent with Section VI.A.1 of the NRC
air. The licensee entered the issue into its CAP as CR 03-06556. Because this violation
  Enforcement Policy. (NCV 05000346/2003010-11)
was of very low safety significance and because it was entered into the licensees CAP,
.5 Inadequate Blowdown Provisions for Containment Isolation Valve Accumulators
this violation is being treated as an NCV consistent with Section VI.A.1 of the NRC
  Introduction: The team identified a performance deficiency involving the licensee's
Enforcement Policy. (NCV 05000346/2003010-11)
  failure to initiate a CR or to implement corrective actions to address a previously
    .5
  identified NRC finding. Following discovery, the licensee entered the issue into its
Inadequate Blowdown Provisions for Containment Isolation Valve Accumulators  
  corrective action program.
Introduction: The team identified a performance deficiency involving the licensee's
  Description: Non-Cited Violation 05000346/2002014-01b was issued by the NRC during
failure to initiate a CR or to implement corrective actions to address a previously
  the 2002 SSDI to document that there were no provisions to blow down the SW
identified NRC finding. Following discovery, the licensee entered the issue into its
  containment isolation valve accumulators although USAR Section 9.3.1.5 stated that the
corrective action program.  
  accumulators contained a provision to allow removal of excessive moisture. IR
Description: Non-Cited Violation 05000346/2002014-01b was issued by the NRC during
  54-346/2002014 documented that this NCV was captured in the licensee's CAP as
the 2002 SSDI to document that there were no provisions to blow down the SW
  CR 02-07750. When the CATI team reviewed CR 02-07750, the team determined that
containment isolation valve accumulators although USAR Section 9.3.1.5 stated that the
  the CR did not document this concern. The licensee was unable to identify any CR
accumulators contained a provision to allow removal of excessive moisture. IR
  which addressed the NCV and could not find any indication that corrective actions had
54-346/2002014 documented that this NCV was captured in the licensee's CAP as
  been taken to address the issue.
CR 02-07750. When the CATI team reviewed CR 02-07750, the team determined that
  The valves discussed in the NCV were containment isolation valves equipped with
the CR did not document this concern. The licensee was unable to identify any CR
  backup air accumulators (air volume tanks). These valves had dual safety functions in
which addressed the NCV and could not find any indication that corrective actions had
  that they were required to open during a LOCA to provide maximum SW flow through
been taken to address the issue.
  the CACs as well as being required to close to provide containment isolation. The team
The valves discussed in the NCV were containment isolation valves equipped with
  noted that, although the licensee was in the process of designing the new accumulators,
backup air accumulators (air volume tanks). These valves had dual safety functions in
  they had not specifically considered or addressed providing accumulator blowdown
that they were required to open during a LOCA to provide maximum SW flow through
  capability. The failure to include blowdown provisions meant that any moisture intrusion
the CACs as well as being required to close to provide containment isolation. The team
  into the accumulator would not be identifiable and would not be removable. This would
noted that, although the licensee was in the process of designing the new accumulators,
  result in the reduction in the amount of air available to maintain the containment
they had not specifically considered or addressed providing accumulator blowdown
  isolation valves closed and would result in rust and other debris in the accumulator.
capability. The failure to include blowdown provisions meant that any moisture intrusion
  In response to the teams finding, the licensee issued CR 03-02475 on March 28, 2003,
into the accumulator would not be identifiable and would not be removable. This would
  to document this concern and ensure that it was included in the Davis-Besse CAP. The
result in the reduction in the amount of air available to maintain the containment
  licensee informed the team that MOD 99-0039, Revision 1 should address this concern,
isolation valves closed and would result in rust and other debris in the accumulator.
  when completed. In November 2003, the team reviewed the corrective actions
In response to the teams finding, the licensee issued CR 03-02475 on March 28, 2003,
  generated for CR 03-02475 and determined that the specified modification had been
to document this concern and ensure that it was included in the Davis-Besse CAP. The
  canceled and a new modification package generated. Based on the wording in the
licensee informed the team that MOD 99-0039, Revision 1 should address this concern,
  corrective action cancellation, it was not apparent that the blowdown issue was
when completed. In November 2003, the team reviewed the corrective actions
  reassessed as part of the new modification.
generated for CR 03-02475 and determined that the specified modification had been
  The team independently determined that, due to the change in accumulator medium
canceled and a new modification package generated. Based on the wording in the
  from air to nitrogen, that there was no longer any need for blowdown provisions. While
corrective action cancellation, it was not apparent that the blowdown issue was
  the NRC concluded that the lack of blowdown no longer presented a safety issue.
reassessed as part of the new modification.
                                            47                                    Enclosure
The team independently determined that, due to the change in accumulator medium
from air to nitrogen, that there was no longer any need for blowdown provisions. While
the NRC concluded that the lack of blowdown no longer presented a safety issue.


  Analysis: The team determined that a performance deficiency existed because the
Enclosure
  licensees program required it to initiate a CR and implement corrective actions to
48
  address NRC identified NCVs. Since there was a performance deficiency, the team
Analysis: The team determined that a performance deficiency existed because the
  compared this performance deficiency to the minor questions contained in Appendix B,
licensees program required it to initiate a CR and implement corrective actions to
  "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
address NRC identified NCVs. Since there was a performance deficiency, the team
  concluded that the issue was minor because the licensee changed the accumulator
compared this performance deficiency to the minor questions contained in Appendix B,
  medium to one which would not contain moisture, such that the failure to take corrective
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
  actions had no consequences.
concluded that the issue was minor because the licensee changed the accumulator
  Enforcement: The failure to take corrective actions for an identified condition adverse to
medium to one which would not contain moisture, such that the failure to take corrective
  quality constituted a violation of 10 CFR Appendix B, Criterion XVI, which has minor
actions had no consequences.
  significance and is not subject to enforcement action in accordance with Section IV of
Enforcement: The failure to take corrective actions for an identified condition adverse to
  the NRCs Enforcement Policy.
quality constituted a violation of 10 CFR Appendix B, Criterion XVI, which has minor
  While minor violations are not normally documented in inspection reports, the team
significance and is not subject to enforcement action in accordance with Section IV of
  determined that documentation was appropriate in this case due to the issue not initially
the NRCs Enforcement Policy.  
  being in the CAP and then due to the corrective actions being canceled without
While minor violations are not normally documented in inspection reports, the team
  reconciliation of the original issue. Additionally, the underlying cause is similar to that of
determined that documentation was appropriate in this case due to the issue not initially
  other findings in this report.
being in the CAP and then due to the corrective actions being canceled without
.6 Non-conservative Calculation Used in Design Analysis to Determine Required
reconciliation of the original issue. Additionally, the underlying cause is similar to that of
  Service Water Makeup Flow to Component Cooling Water
other findings in this report.
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    .6
  having very low safety significance. Specifically, the licensee failed to consider worst
Non-conservative Calculation Used in Design Analysis to Determine Required
  case minimum pressure differential between SW and component cooling water (CCW)
Service Water Makeup Flow to Component Cooling Water
  systems when determining required SW makeup flow to the CCW system heat
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  exchangers. Following discovery, the licensee entered the issue into its corrective
having very low safety significance. Specifically, the licensee failed to consider worst
  action process and performed the necessary calculations. The primary cause of this
case minimum pressure differential between SW and component cooling water (CCW)
  violation was related to the cross-cutting area of human performance because the
systems when determining required SW makeup flow to the CCW system heat
  licensee used test data collected during normal operation rather than taking the worst
exchangers. Following discovery, the licensee entered the issue into its corrective
  case design conditions and because there was a lack of rigor in the calculation review
action process and performed the necessary calculations. The primary cause of this
  process.
violation was related to the cross-cutting area of human performance because the
  Description: Hydraulic calculation C-ME-011.01-140 was developed as part of a
licensee used test data collected during normal operation rather than taking the worst
  corrective action to CR 02-07378. This calculation determined the pressure differential
case design conditions and because there was a lack of rigor in the calculation review
  required in the SW line for makeup to the CCW system to create a minimum flow of
process.
  30 gpm. This flowrate was used to estimate the stay time and exposure rate while using
Description: Hydraulic calculation C-ME-011.01-140 was developed as part of a
  SW to makeup to the CCW system. The NRC team reviewed the calculation, and
corrective action to CR 02-07378. This calculation determined the pressure differential
  determined that it was non-conservative in that it did not consider worst-case minimum
required in the SW line for makeup to the CCW system to create a minimum flow of  
  pressure differential between SW and CCW systems during accident conditions, but
30 gpm. This flowrate was used to estimate the stay time and exposure rate while using
  used test data collected during normal operation. In addition, the calculation assumed a
SW to makeup to the CCW system. The NRC team reviewed the calculation, and
  fully turbulent fouling factor for clean piping. Finally, there was a minor math error in the
determined that it was non-conservative in that it did not consider worst-case minimum
  calculation. Although the math error did not appreciably affect the results of the
pressure differential between SW and CCW systems during accident conditions, but
  calculation, it indicated a lack of rigor in the calculation review process. In response to
used test data collected during normal operation. In addition, the calculation assumed a
  the NRC's questions, the licensee performed additional calculations. The licensee
fully turbulent fouling factor for clean piping. Finally, there was a minor math error in the
  stated that these new calculations showed that, even with the lower predicted differential
calculation. Although the math error did not appreciably affect the results of the
  pressures while in the accident alignment, the makeup capability of SW to CCW
calculation, it indicated a lack of rigor in the calculation review process. In response to
                                              48                                      Enclosure
the NRC's questions, the licensee performed additional calculations. The licensee
stated that these new calculations showed that, even with the lower predicted differential
pressures while in the accident alignment, the makeup capability of SW to CCW


  exceeded the acceptance criteria. The team did not review these additional
Enclosure
  calculations.
49
  Analysis: The team determined that a performance deficiency existed because the
exceeded the acceptance criteria. The team did not review these additional
  licensee failed to verify the adequacy of the design basis calculation performed for the
calculations.
  SW and CCW system interface. Since there was a performance deficiency, the team
Analysis: The team determined that a performance deficiency existed because the
  compared this performance deficiency to the minor questions contained in Appendix B,
licensee failed to verify the adequacy of the design basis calculation performed for the
  "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
SW and CCW system interface. Since there was a performance deficiency, the team
  concluded that the issue was more than minor because the licensee had to perform a
compared this performance deficiency to the minor questions contained in Appendix B,
  new calculation to demonstrate that the SW flow to CCW was adequate to perform its
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
  design function. This finding was considered a design deficiency which affected the
concluded that the issue was more than minor because the licensee had to perform a
  mitigating systems cornerstone. The licensee determined that the SW flow was
new calculation to demonstrate that the SW flow to CCW was adequate to perform its
  adequate to perform its design function and was operable The team reviewed this
design function. This finding was considered a design deficiency which affected the
  finding in accordance with IMC 0609, "Significance Determination Process, and
mitigating systems cornerstone. The licensee determined that the SW flow was
  answered no to all five screening questions in the Phase 1 Screening Worksheet
adequate to perform its design function and was operable The team reviewed this
  under the Mitigating Systems column. The team concluded the issue was of very low
finding in accordance with IMC 0609, "Significance Determination Process, and
  safety significance (Green).
answered no to all five screening questions in the Phase 1 Screening Worksheet
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
under the Mitigating Systems column. The team concluded the issue was of very low
  measures be established to assure that applicable regulatory requirements and the
safety significance (Green).
  design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
  instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
  checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
  use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
  testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
  Contrary to the above, the licensee failed to implement design control measures to
use of alternate or simplified calculational methods, or by the performance of a suitable
  check and verify the adequacy of the design basis calculation performed for the
testing program.
  SW/CCW system crosstie hydraulic analyses for all postulated accidents. The licensee
Contrary to the above, the licensee failed to implement design control measures to
  entered the issue into its CAP as CR 03-04010. Because this violation was of very low
check and verify the adequacy of the design basis calculation performed for the
  safety significance and because it was entered into the licensees CAP, the violation is
SW/CCW system crosstie hydraulic analyses for all postulated accidents. The licensee
  being treated as a NCV, consistent with Section VI.A of the NRC Enforcement Policy.
entered the issue into its CAP as CR 03-04010. Because this violation was of very low
  (NCV 05000346/2003010-12)
safety significance and because it was entered into the licensees CAP, the violation is
.7 Calculation Concerns for Service Water Pump Room Ventilation System
being treated as a NCV, consistent with Section VI.A of the NRC Enforcement Policy.  
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
(NCV 05000346/2003010-12)
  having very low safety significance (Green). Specifically, the licensee failed to verify the
    .7
  adequacy of the design of the SW pump room ventilation system. Following discovery
Calculation Concerns for Service Water Pump Room Ventilation System
  that the design basis calculations were non-conservative, the licensee entered the issue
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  into its corrective action program, re-performed the calculations, and made appropriate
having very low safety significance (Green). Specifically, the licensee failed to verify the
  modifications to correct the issues. The primary cause of this violation was related to
adequacy of the design of the SW pump room ventilation system. Following discovery
  the cross-cutting area of problem identification and resolution because the licensee
that the design basis calculations were non-conservative, the licensee entered the issue
  failed to correct all of the originally identified issues until identified by team.
into its corrective action program, re-performed the calculations, and made appropriate
  Description: During the SSDI inspection in 2002, the NRC identified a concern
modifications to correct the issues. The primary cause of this violation was related to
  regarding calculation 67.005. The calculation analyzed the heat loads in the SW pump
the cross-cutting area of problem identification and resolution because the licensee
  room and the ability of the ventilation system to maintain the pump room temperatures
failed to correct all of the originally identified issues until identified by team.
  within a required operating range. The team determined that the calculation contained
Description: During the SSDI inspection in 2002, the NRC identified a concern
                                              49                                      Enclosure
regarding calculation 67.005. The calculation analyzed the heat loads in the SW pump
 
room and the ability of the ventilation system to maintain the pump room temperatures
multiple non-conservative attributes, including failing to analyze heat loss through open
within a required operating range. The team determined that the calculation contained
penthouse louvers during the winter, and failing to account for heat load contribution of
 
diesel driven fire pump during the summer. The licensee initiated CR 02-07188 to
Enclosure
50
multiple non-conservative attributes, including failing to analyze heat loss through open
penthouse louvers during the winter, and failing to account for heat load contribution of
diesel driven fire pump during the summer. The licensee initiated CR 02-07188 to
document this issue.
document this issue.
The calculation was revised to address these concerns and was issued as Revision 4 in
The calculation was revised to address these concerns and was issued as Revision 4 in
early 2003. At the same time, another CR, 02-08281, was issued because
early 2003. At the same time, another CR, 02-08281, was issued because
CR 02-07188 failed to do an extent of condition review to verify the adequacy of the SW
CR 02-07188 failed to do an extent of condition review to verify the adequacy of the SW
ventilation system for all operating conditions. The extent of condition review was
ventilation system for all operating conditions. The extent of condition review was
reported to have included a walkdown of the SW pump room and review of the revised
reported to have included a walkdown of the SW pump room and review of the revised
SW ventilation calculation.
SW ventilation calculation.
Line 2,697: Line 3,062:
maximum analyzed temperature in the pump house did not include the heat load
maximum analyzed temperature in the pump house did not include the heat load
contribution of the diesel driven fire pump, which was one of the deficiencies noted in
contribution of the diesel driven fire pump, which was one of the deficiencies noted in
the earlier revision to the calculation. This deficiency was not addressed in the new
the earlier revision to the calculation. This deficiency was not addressed in the new
revision to the calculation, either by including it or by providing a rationale for excluding
revision to the calculation, either by including it or by providing a rationale for excluding
the heat load. The team noted that the licensee had previously had to take actions to
the heat load. The team noted that the licensee had previously had to take actions to
open the diesel generator room doors and provide alternate ventilation during the
open the diesel generator room doors and provide alternate ventilation during the
summer months. The new calculation also concluded that the penthouse louvers had to
summer months. The new calculation also concluded that the penthouse louvers had to
be modified (blocked) for winter operation. The NRC team noted that past operability
be modified (blocked) for winter operation. The NRC team noted that past operability
had been assured for winter operation by regularly recording pump room ambient
had been assured for winter operation by regularly recording pump room ambient
temperature.
temperature.
Calculation C-NSA-085.00-002, Auxiliary Steam Blowdown in the Intake Structure,
Calculation C-NSA-085.00-002, Auxiliary Steam Blowdown in the Intake Structure,
concluded that the maximum temperature within the SW pump room was 109
concluded that the maximum temperature within the SW pump room was 109
degrees F. This temperature was not considered a significant difference from the
degrees F. This temperature was not considered a significant difference from the
normal operating temperature in the room. Additionally, the safety related equipment in
normal operating temperature in the room. Additionally, the safety related equipment in
the room was specified for operation in an environment with 100 percent relative
the room was specified for operation in an environment with 100 percent relative
humidity, which would be experienced in the room during a postulated steam break. An
humidity, which would be experienced in the room during a postulated steam break. An
evaluation performed in CR 02-05262 concluded that the amount of condensing
evaluation performed in CR 02-05262 concluded that the amount of condensing
moisture would fill the smallest electrical junction box by only 0.05 inches. Therefore,
moisture would fill the smallest electrical junction box by only 0.05 inches. Therefore,
the functionality of the cables and connections was not likely to be affected. The team
the functionality of the cables and connections was not likely to be affected. The team
also noted that the licensee had initiated engineering change request (ECR) 02-0682 to
also noted that the licensee had initiated engineering change request (ECR) 02-0682 to
remove the auxiliary steam line from the SW pump room, although it stated that this
remove the auxiliary steam line from the SW pump room, although it stated that this
modification was an enhancement which was not required.
modification was an enhancement which was not required.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to verify the adequacy of the SW pump room ventilation system for all
licensee failed to verify the adequacy of the SW pump room ventilation system for all
operating conditions. Since there was a performance deficiency, the team compared this
operating conditions. Since there was a performance deficiency, the team compared this
performance deficiency to the minor questions contained in Appendix B, "Issue
performance deficiency to the minor questions contained in Appendix B, "Issue
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded that
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded that
the issue was more than minor because inadequacies in the calculations identified during
the issue was more than minor because inadequacies in the calculations identified during
the 2002 SSDI resulted in a modification to ensure winter operation was within the
the 2002 SSDI resulted in a modification to ensure winter operation was within the
allowable temperature range, and because the revised calculation did not include all the
allowable temperature range, and because the revised calculation did not include all the
summer heat loads which could potentially impair the SW pump room ventilation system.
summer heat loads which could potentially impair the SW pump room ventilation system.  
This was a design issue which affected the mitigating systems cornerstone. The team
This was a design issue which affected the mitigating systems cornerstone. The team
reviewed this finding in accordance with IMC 0609, "Significance Determination Process,
reviewed this finding in accordance with IMC 0609, "Significance Determination Process,
and answered no to all five screening questions in the Phase 1 Screening Worksheet
and answered no to all five screening questions in the Phase 1 Screening Worksheet
                                          50                                        Enclosure


  under the Mitigating Systems column. The team concluded the issue was of very low
Enclosure
  safety significance (Green).
51
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
under the Mitigating Systems column. The team concluded the issue was of very low
  measures be established to assure that applicable regulatory requirements and the
safety significance (Green).
  design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
  instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
  checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
  use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
  testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
  Contrary to the above, the licensee failed to implement design control measures to
use of alternate or simplified calculational methods, or by the performance of a suitable
  check and verify the adequacy of the design. Specifically, the licensee failed to verify
testing program.
  the adequacy of the SW pump room ventilation system for all operating conditions.
Contrary to the above, the licensee failed to implement design control measures to
  The licensee entered this issue into its CAP as CRs 02-07188 and 03-06870. Because
check and verify the adequacy of the design. Specifically, the licensee failed to verify
  this violation was of very low safety significance and because it was entered into the
the adequacy of the SW pump room ventilation system for all operating conditions.
  licensees CAP, this violation is being treated as a NCV consistent with Section VI.A.1 of
The licensee entered this issue into its CAP as CRs 02-07188 and 03-06870. Because
  the NRC Enforcement Policy. (NCV 05000346/2003010-13)
this violation was of very low safety significance and because it was entered into the
.8 Inadequate Service Water System Flow Analysis
licensees CAP, this violation is being treated as a NCV consistent with Section VI.A.1 of
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
the NRC Enforcement Policy. (NCV 05000346/2003010-13)
  having very low safety significance. Specifically, the licensee failed to ensure that the
    .8
  SW system could perform its design function under all required conditions. Following
Inadequate Service Water System Flow Analysis
  discovery, the licensee entered the issue into its corrective action program and
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  performed the necessary calculations.
having very low safety significance. Specifically, the licensee failed to ensure that the
  Description: In IR 05000346/2002014, several URIs were identified dealing with the SW
SW system could perform its design function under all required conditions. Following
  system and ultimate heat sinks. These deficiencies included failure to account for the
discovery, the licensee entered the issue into its corrective action program and
  lowest acceptable performance of the SW pumps, failure to consider the USAR
performed the necessary calculations.
  described single failure of the forebay return valve to open, failure to include the design
Description: In IR 05000346/2002014, several URIs were identified dealing with the SW
  basis strainer resistance, and strainer blowdown losses. Additionally, the design basis
system and ultimate heat sinks. These deficiencies included failure to account for the
  lowest ultimate heat sink level was not used and the flow diverted to the AFW was not
lowest acceptable performance of the SW pumps, failure to consider the USAR
  considered. Because of these deficiencies, the ability of the system to provide the
described single failure of the forebay return valve to open, failure to include the design
  required design basis flows to the safety-related heat exchangers could not be verified.
basis strainer resistance, and strainer blowdown losses. Additionally, the design basis
  In response to the issues identified by the SSDI, as well as other issues identified
lowest ultimate heat sink level was not used and the flow diverted to the AFW was not
  internally, the licensee determined that there was not sufficient design basis
considered. Because of these deficiencies, the ability of the system to provide the
  documentation to demonstrate operability of the SW system under all required
required design basis flows to the safety-related heat exchangers could not be verified.
  conditions. The licensee had a consultant perform two new calculations, 02-113 and
In response to the issues identified by the SSDI, as well as other issues identified
  02-123, to address a large number of SW flow issues, including those issues discussed
internally, the licensee determined that there was not sufficient design basis
  above.
documentation to demonstrate operability of the SW system under all required
  The team reviewed these calculations and noted that the calculations determined that,
conditions. The licensee had a consultant perform two new calculations, 02-113 and
  under a certain combination of design basis conditions, design basis flow rates and
02-123, to address a large number of SW flow issues, including those issues discussed
  pump net positive suction head (NPSH) were not achievable. The specific combination
above.
  included having design basis low ultimate heat sink levels, design basis high SW
The team reviewed these calculations and noted that the calculations determined that,
  temperatures and the SW strainers going into backwash while the system was
under a certain combination of design basis conditions, design basis flow rates and
                                            51                                      Enclosure
pump net positive suction head (NPSH) were not achievable. The specific combination
included having design basis low ultimate heat sink levels, design basis high SW
temperatures and the SW strainers going into backwash while the system was


responding to a design basis accident. The team determined that the strainer operation
Enclosure
52
responding to a design basis accident. The team determined that the strainer operation
was automatic such that this set of circumstances was one which the licensee should
was automatic such that this set of circumstances was one which the licensee should
have included as part of its design basis.
have included as part of its design basis.
The team noted that the licensee had reviewed and approved the calculation without
The team noted that the licensee had reviewed and approved the calculation without
comment. This issue negatively reflected on the adequacy of the licensees engineering
comment. This issue negatively reflected on the adequacy of the licensees engineering
department to oversee the engineering contractor performing the calculations and on
department to oversee the engineering contractor performing the calculations and on
the engineering staffs ability to identify engineering issues and non-conforming
the engineering staffs ability to identify engineering issues and non-conforming
conditions. The team independently evaluated the issue and determined that the
conditions. The team independently evaluated the issue and determined that the
system would most likely be able to perform its design function as the inadequate
system would most likely be able to perform its design function as the inadequate
conditions would only exist for short periods of time. The licencee initiated CR 03-03977
conditions would only exist for short periods of time. The licencee initiated CR 03-03977
to revise the calculations. Following evaluation of CR 03-03977, the licensee concluded
to revise the calculations. Following evaluation of CR 03-03977, the licensee concluded
that the SW system was able to perform its safety related function. The team agreed
that the SW system was able to perform its safety related function. The team agreed
with the licensees conclusions.
with the licensees conclusions.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to ensure the adequacy of the SW system to supply required flow rate to
licensee failed to ensure the adequacy of the SW system to supply required flow rate to
safety related components and failed to ensure the required NPSH for the SW pumps.
safety related components and failed to ensure the required NPSH for the SW pumps.  
Since there was a performance deficiency, the team compared this performance
Since there was a performance deficiency, the team compared this performance
deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
0612, "Power Reactor Inspection Reports." The team concluded that the issue was
0612, "Power Reactor Inspection Reports." The team concluded that the issue was
more than minor because the licensee did not initially have a calculation which
more than minor because the licensee did not initially have a calculation which
demonstrated that the SW system could fulfill its design function under design basis
demonstrated that the SW system could fulfill its design function under design basis
conditions and when a calculation was subsequently prepared, system deficiencies were
conditions and when a calculation was subsequently prepared, system deficiencies were
not evaluated to ensure that the safety function could be met. This was a design issue
not evaluated to ensure that the safety function could be met. This was a design issue
which affected the mitigating systems cornerstone. The licensee concluded that the SW
which affected the mitigating systems cornerstone. The licensee concluded that the SW
system had been able to perform its safety function. The team reviewed this finding in
system had been able to perform its safety function. The team reviewed this finding in
accordance with IMC 0609, "Significance Determination Process, and answered no to
accordance with IMC 0609, "Significance Determination Process, and answered no to
all five screening questions in the Phase 1 Screening Worksheet under the Mitigating
all five screening questions in the Phase 1 Screening Worksheet under the Mitigating
Systems column. The team concluded the issue was of very low safety significance
Systems column. The team concluded the issue was of very low safety significance
(Green).
(Green).
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
measures be established to assure that applicable regulatory requirements and the
measures be established to assure that applicable regulatory requirements and the
design basis were correctly translated into specifications, drawings, procedures, and
design basis were correctly translated into specifications, drawings, procedures, and
instructions. Furthermore, it requires that measures be provided for verifying or
instructions. Furthermore, it requires that measures be provided for verifying or
checking the adequacy of design, such as by the performance of design reviews, by the
checking the adequacy of design, such as by the performance of design reviews, by the
use of alternate or simplified calculational methods, or by the performance of a suitable
use of alternate or simplified calculational methods, or by the performance of a suitable
testing program.
testing program.
Contrary to the above, the licensee failed to ensure that design requirements were
Contrary to the above, the licensee failed to ensure that design requirements were
correctly translated into specifications, drawings, procedures, and instructions.
correctly translated into specifications, drawings, procedures, and instructions.  
Specifically, the licensee did not have design calculations to show the SW system could
Specifically, the licensee did not have design calculations to show the SW system could
perform its required safety function under design basis conditions.
perform its required safety function under design basis conditions.
The licensee entered the issue into its CAP as CRs 02-06337, 03-07006, and 03-07042.
The licensee entered the issue into its CAP as CRs 02-06337, 03-07006, and 03-07042.  
Because this violation was of very low safety significance and because it was entered
Because this violation was of very low safety significance and because it was entered
into the licensee CAP, this violation is being treated as a NCV, consistent with
into the licensee CAP, this violation is being treated as a NCV, consistent with  
Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000346/2003010-14)
Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000346/2003010-14)
                                            52                                    Enclosure


.9 Inadequate Flooding Protection for the Service Water System
Enclosure
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
53
  having very low safety significance (Green). Specifically, the licensee failed to have
    .9
  provisions in place to protect the SW pump room from flooding. Following discovery,
Inadequate Flooding Protection for the Service Water System
  the licensee placed the issue in its corrective action program, evaluated it and put
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
  procedures in place to address the issue.
having very low safety significance (Green). Specifically, the licensee failed to have
  Description: During the SSDI in 2002, the NRC identified that no procedures were in
provisions in place to protect the SW pump room from flooding. Following discovery,
  place to isolate equipment open for maintenance in the SW pump room that could flood
the licensee placed the issue in its corrective action program, evaluated it and put
  the room in the event of high lake water level. USAR Section 2.4.8.2 stated, "The
procedures in place to address the issue.
  Probable Maximum Flood Water is elevation 583.7 feet..." USAR Section 9.2.1.3
Description: During the SSDI in 2002, the NRC identified that no procedures were in
  stated, "In the event of high water levels,...the pump room is sealed to prevent flooding."
place to isolate equipment open for maintenance in the SW pump room that could flood
  Finally USAR Section 3D.1.4, "[General Design Criteria (GDC)] Criterion IV -
the room in the event of high lake water level. USAR Section 2.4.8.2 stated, "The
  Environmental and Missile Design Basis," stated, "These [safety-related] structures,
Probable Maximum Flood Water is elevation 583.7 feet..." USAR Section 9.2.1.3
  systems, and components are appropriately protected against dynamic effects...and
stated, "In the event of high water levels,...the pump room is sealed to prevent flooding."
  discharging fluids, that may result from equipment failures and from events and
Finally USAR Section 3D.1.4, "[General Design Criteria (GDC)] Criterion IV -
  conditions outside the nuclear power unit." Therefore, the NRC questioned whether the
Environmental and Missile Design Basis," stated, "These [safety-related] structures,
  SW system was adequately protected against flooding effects that could result from
systems, and components are appropriately protected against dynamic effects...and
  high lake water levels, from internal flooding, and from other threats to the system that
discharging fluids, that may result from equipment failures and from events and
  could result from failure of non-seismically qualified equipment, as described in the
conditions outside the nuclear power unit." Therefore, the NRC questioned whether the
  USAR.
SW system was adequately protected against flooding effects that could result from
  In response to this concern, the licensee determined that operator actions were
high lake water levels, from internal flooding, and from other threats to the system that
  necessary in order to ensure that the USAR statements were met. In order to ensure
could result from failure of non-seismically qualified equipment, as described in the
  that the operator actions occurred, several changes to operating procedures were
USAR.
  required. These procedural actions were taken. During the 2003 CATI, the team
In response to this concern, the licensee determined that operator actions were
  verified that the corrective actions were implemented and appropriately resolved.
necessary in order to ensure that the USAR statements were met. In order to ensure
  Analysis: The team determined that a performance deficiency existed because the
that the operator actions occurred, several changes to operating procedures were
  licensee failed to translate design basis requirements into procedures for flood
required. These procedural actions were taken. During the 2003 CATI, the team
  protection in the SW pump room. Since there was a performance deficiency, the team
verified that the corrective actions were implemented and appropriately resolved.
  compared this performance deficiency to the minor questions contained in Appendix B,
Analysis: The team determined that a performance deficiency existed because the
  "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
licensee failed to translate design basis requirements into procedures for flood
  concluded that the issue was more than minor because the licensee had to make
protection in the SW pump room. Since there was a performance deficiency, the team
  procedural changes in order to ensure that safety-related equipment was capable of
compared this performance deficiency to the minor questions contained in Appendix B,
  performing its safety functions. This was a procedural deficiency which affected the
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
  mitigating systems cornerstone. The licensee determined that the system remained
concluded that the issue was more than minor because the licensee had to make
  operable since the deficiency only dealt with a lack of procedural guidance. The team
procedural changes in order to ensure that safety-related equipment was capable of
  reviewed this finding in accordance with IMC 0609, "Significance Determination
performing its safety functions. This was a procedural deficiency which affected the
  Process, and answered no to all five screening questions in the Phase 1 Screening
mitigating systems cornerstone. The licensee determined that the system remained
  Worksheet under the Mitigating Systems column. The team concluded the issue was of
operable since the deficiency only dealt with a lack of procedural guidance. The team
  very low safety significance (Green).
reviewed this finding in accordance with IMC 0609, "Significance Determination
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
Process, and answered no to all five screening questions in the Phase 1 Screening
  measures be established to assure that applicable regulatory requirements and the
Worksheet under the Mitigating Systems column. The team concluded the issue was of
  design basis were correctly translated into specifications, drawings, procedures, and
very low safety significance (Green).
  instructions. Furthermore, it requires that measures be provided for verifying or
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
  checking the adequacy of design, such as by the performance of design reviews, by the
measures be established to assure that applicable regulatory requirements and the
                                            53                                      Enclosure
design basis were correctly translated into specifications, drawings, procedures, and
instructions. Furthermore, it requires that measures be provided for verifying or
checking the adequacy of design, such as by the performance of design reviews, by the


    use of alternate or simplified calculational methods, or by the performance of a suitable
Enclosure
    testing program.
54
    Contrary to the above, the licensee failed to correctly translate the design basis into
use of alternate or simplified calculational methods, or by the performance of a suitable
    procedures. Specifically, the licensee failed to have procedures in place to isolate
testing program.
    equipment opened during maintenance in the SW pump room that could potentially
Contrary to the above, the licensee failed to correctly translate the design basis into
    flood the room in the event of rising lake water level.
procedures. Specifically, the licensee failed to have procedures in place to isolate
    The licensee had previously entered this issue into its CAP as CR 02-07714. Because
equipment opened during maintenance in the SW pump room that could potentially
    this violation was of very low safety significance and because it was entered into the
flood the room in the event of rising lake water level.
    licensees CAP, the violation is being treated as a NCV, consistent with Section VI.A of
The licensee had previously entered this issue into its CAP as CR 02-07714. Because
    the NRC Enforcement Policy. (NCV 05000346/2003010-15)
this violation was of very low safety significance and because it was entered into the
.10 Inadequate Service Water System Flow Balance Testing Procedure
licensees CAP, the violation is being treated as a NCV, consistent with Section VI.A of
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,
the NRC Enforcement Policy. (NCV 05000346/2003010-15)
    having very low safety significance (Green). Specifically, the licensee failed to account
    .10 Inadequate Service Water System Flow Balance Testing Procedure
    for a number of conditions in the SW system flow balance testing procedures. Following
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,
    discovery, the licensee placed the issue in its corrective action program, evaluated it and
having very low safety significance (Green). Specifically, the licensee failed to account
    put procedures in place to address the issue.
for a number of conditions in the SW system flow balance testing procedures. Following
    Description: Surveillance procedures DB-SP-03000 and 03001, "Service Water
discovery, the licensee placed the issue in its corrective action program, evaluated it and
    Integrated Train I (II) Flow Balance Procedure," were performed every refueling outage
put procedures in place to address the issue.
    to balance the system flows. During the 2002 SSDI, the NRC identified that this
Description: Surveillance procedures DB-SP-03000 and 03001, "Service Water
    procedure did not establish flows to the safety-related heat exchangers based on
Integrated Train I (II) Flow Balance Procedure," were performed every refueling outage
    worst-case design basis conditions, such as degraded SW pumps, lowest ultimate heat
to balance the system flows. During the 2002 SSDI, the NRC identified that this
    sink (UHS) level, highest resistance SW system lineup, or system resistance
procedure did not establish flows to the safety-related heat exchangers based on
    degradation. Further, no analyses existed that established the test acceptance criteria
worst-case design basis conditions, such as degraded SW pumps, lowest ultimate heat
    for design basis conditions. Therefore, the flow balance procedure did not verify that
sink (UHS) level, highest resistance SW system lineup, or system resistance
    the system was capable of providing the required flows to its safety-related heat
degradation. Further, no analyses existed that established the test acceptance criteria
    exchangers under design basis conditions.
for design basis conditions. Therefore, the flow balance procedure did not verify that
    The licensee performed SW flow model calculations that conservatively predicted the
the system was capable of providing the required flows to its safety-related heat
    required flow to each safety-related load. The model addressed all SW branch lines in
exchangers under design basis conditions.
    service during various accident scenarios and accounted for the flow rate issues
The licensee performed SW flow model calculations that conservatively predicted the
    described in CR 02-06337. Separately, the licensee computed the required instrument
required flow to each safety-related load. The model addressed all SW branch lines in
    inaccuracies for the instrumentation used during the SW flow balance.
service during various accident scenarios and accounted for the flow rate issues
    However, the licensee's design organization did not ensure that this information was
described in CR 02-06337. Separately, the licensee computed the required instrument
    properly transmitted to the plant engineering group in a format that would ensure that
inaccuracies for the instrumentation used during the SW flow balance.
    the procedures had adequate acceptance criteria. The design engineering organization
However, the licensee's design organization did not ensure that this information was
    did not perform a formal calculation which documented the minimum acceptance criteria
properly transmitted to the plant engineering group in a format that would ensure that
    to ensure that the test procedure would demonstrate that the SW flows met their design
the procedures had adequate acceptance criteria. The design engineering organization
    basis requirements. Instead, design engineering transmitted the design information in
did not perform a formal calculation which documented the minimum acceptance criteria
    two separate evaluations which then had to be combined by plant engineering and
to ensure that the test procedure would demonstrate that the SW flows met their design
    corrected for the instrument measurement uncertainty. Because the plant engineering
basis requirements. Instead, design engineering transmitted the design information in
    department had to interpret the results from design engineering, the plant engineering
two separate evaluations which then had to be combined by plant engineering and
    personnel applied considerable conservatism when establishing the test acceptance
corrected for the instrument measurement uncertainty. Because the plant engineering
                                              54                                    Enclosure
department had to interpret the results from design engineering, the plant engineering
personnel applied considerable conservatism when establishing the test acceptance


criteria. The licensee issued CR 03-07006 to provide a design record file for test
Enclosure
55
criteria. The licensee issued CR 03-07006 to provide a design record file for test
acceptance criteria.
acceptance criteria.
During SW testing performed in the summer and fall 2003, the licensee determined that
During SW testing performed in the summer and fall 2003, the licensee determined that
the newly established test acceptance criteria could not be met for some components.
the newly established test acceptance criteria could not be met for some components.  
This resulted in numerous CRs being written and the design engineering organization
This resulted in numerous CRs being written and the design engineering organization
having to prepare a number of operability evaluations justifying the use of lower
having to prepare a number of operability evaluations justifying the use of lower
acceptance criteria. The team determined that the design engineering failure to
acceptance criteria. The team determined that the design engineering failure to
establish appropriate acceptance criteria prior to the SW testing occurring contributed to
establish appropriate acceptance criteria prior to the SW testing occurring contributed to
the number of CRs and subsequent operability evaluations.
the number of CRs and subsequent operability evaluations.
The team determined that the licensee planned to perform a flow balance twice each
The team determined that the licensee planned to perform a flow balance twice each
refueling outage, once on as found basis, and once on an as-left basis. Collecting
refueling outage, once on as found basis, and once on an as-left basis. Collecting
as-found data would provide evidence that the SW system branch flows were adequate
as-found data would provide evidence that the SW system branch flows were adequate
during the previous operating cycle to remove the design basis heat loads. The team
during the previous operating cycle to remove the design basis heat loads. The team
considered this a positive step by plant engineering to ensure operability of the SW
considered this a positive step by plant engineering to ensure operability of the SW
system.
system.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to properly account for a number of required conditions in the SW system
licensee failed to properly account for a number of required conditions in the SW system
flow balance testing procedure. Since there was a performance deficiency, the team
flow balance testing procedure. Since there was a performance deficiency, the team
compared this performance deficiency to the minor questions contained in Appendix B,
compared this performance deficiency to the minor questions contained in Appendix B,
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
concluded that the issue was more than minor because procedural changes were
concluded that the issue was more than minor because procedural changes were
necessary in order to ensure that the safety-related SW system branch flow rates were
necessary in order to ensure that the safety-related SW system branch flow rates were
adequate for the system to perform its safety functions. The team assessed the finding
adequate for the system to perform its safety functions. The team assessed the finding
through Phase 1 of the SDP. This was a design issue which affected the mitigating
through Phase 1 of the SDP. This was a design issue which affected the mitigating
systems cornerstone. At the end of the inspection, the licensee was performing a new
systems cornerstone. At the end of the inspection, the licensee was performing a new
flow balance. The licensee concluded that the system was previously capable of
flow balance. The licensee concluded that the system was previously capable of
meeting its design requirements. The flow balance test results were reviewed by the
meeting its design requirements. The flow balance test results were reviewed by the
resident inspectors and document in IR 2003025. The team reviewed this finding in
resident inspectors and document in IR 2003025. The team reviewed this finding in
accordance with IMC 0609, "Significance Determination Process, and answered no to
accordance with IMC 0609, "Significance Determination Process, and answered no to
all five screening questions in the Phase 1 Screening Worksheet under the Mitigating
all five screening questions in the Phase 1 Screening Worksheet under the Mitigating
Systems column. The team concluded the issue was of very low safety significance
Systems column. The team concluded the issue was of very low safety significance
(Green).
(Green).
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI, "Test Control, requires, in
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI, "Test Control, requires, in
part, that a test program shall be established to assure that all testing required to
part, that a test program shall be established to assure that all testing required to
demonstrate that structures, systems, and components will perform satisfactorily in
demonstrate that structures, systems, and components will perform satisfactorily in
Line 2,949: Line 3,321:
Contrary to the above, the licensee failed to adequately test the SW system because
Contrary to the above, the licensee failed to adequately test the SW system because
the licensees SW system flow balance testing procedure failed to account for a number
the licensees SW system flow balance testing procedure failed to account for a number
of required conditions. The testing failed to verify that adequate flow was provided to
of required conditions. The testing failed to verify that adequate flow was provided to
safety related components under all accident conditions.
safety related components under all accident conditions.
                                        55                                      Enclosure


    The licensee entered the issue into its CAP as CRs 02-06064 and 03-07006. Because
Enclosure
    this violation was of very low safety significance and because it was entered into the
56
    licensees CAP, this violation is being treated as a NCV consistent with Section VI.A of
The licensee entered the issue into its CAP as CRs 02-06064 and 03-07006. Because
    the NRC Enforcement Policy. (NCV 05000346/2003010-16)
this violation was of very low safety significance and because it was entered into the
.11 Service Water Discharge Path Swapover Setpoint
licensees CAP, this violation is being treated as a NCV consistent with Section VI.A of
    Introduction: The team identified a violation of 10 CFR Part 50, Appendix B, Criterion III,
the NRC Enforcement Policy. (NCV 05000346/2003010-16)
    involving the licensee's failure to provide a basis for the setpoint to swap the service
    .11 Service Water Discharge Path Swapover Setpoint
    water system discharge path. This issue was previously identified as an NCV in IR
Introduction: The team identified a violation of 10 CFR Part 50, Appendix B, Criterion III,
    05000346/2002014 and the corrective actions taken by the licensee failed to correct the
involving the licensee's failure to provide a basis for the setpoint to swap the service
    originally identified condition. The primary cause of this violation was related to the
water system discharge path. This issue was previously identified as an NCV in IR
    cross-cutting areas of problem identification and resolution and human performance,
05000346/2002014 and the corrective actions taken by the licensee failed to correct the
    because the licensee did not recognize that the corrective actions taken needed to
originally identified condition. The primary cause of this violation was related to the
    restore compliance with the identified violation of NRC requirements.
cross-cutting areas of problem identification and resolution and human performance,
    Description: The 2002 SSDI identified a Green finding and NCV of 10 CFR Part 50,
because the licensee did not recognize that the corrective actions taken needed to
    Appendix B, Criterion III, regarding the licensee's failure to provide a calculational basis
restore compliance with the identified violation of NRC requirements.
    for the 50 psig setpoint to swap SW system discharge path. The licensee did not
Description: The 2002 SSDI identified a Green finding and NCV of 10 CFR Part 50,
    contest the violation and entered the issue into the corrective action system as
Appendix B, Criterion III, regarding the licensee's failure to provide a calculational basis
    CR 02-07802. During the CATI, the team reviewed the evaluation and corrective
for the 50 psig setpoint to swap SW system discharge path. The licensee did not
    actions taken for this NCV. The team determined that the licensee had evaluated the
contest the violation and entered the issue into the corrective action system as
    condition and confirmed that no analysis initially existed. The evaluation reviewed by
CR 02-07802. During the CATI, the team reviewed the evaluation and corrective
    the team was initially approved on March 9, 2003 and had a corrective action also
actions taken for this NCV. The team determined that the licensee had evaluated the
    accepted on March 9, 2003. This evaluation focused on the fact that no setpoint
condition and confirmed that no analysis initially existed. The evaluation reviewed by
    calculation existed which showed that instrument uncertainty values had been properly
the team was initially approved on March 9, 2003 and had a corrective action also
    incorporated, not on providing the calculational basis for the 50 psig setpoint itself. The
accepted on March 9, 2003. This evaluation focused on the fact that no setpoint
    team determined that this evaluation and proposed corrective action were not
calculation existed which showed that instrument uncertainty values had been properly
    responsive to the violation identified during the SSDI.
incorporated, not on providing the calculational basis for the 50 psig setpoint itself. The
    On November 10, 2003, the licensee provided the team a revised copy of CR 02-07802.
team determined that this evaluation and proposed corrective action were not
    The originally approved condition report was apparently rejected and replaced with a
responsive to the violation identified during the SSDI.
    new evaluation and new corrective actions on March 30, 2003. The new evaluation
On November 10, 2003, the licensee provided the team a revised copy of CR 02-07802.
    documented a vendor calculation which showed that with the 50 psig setpoint, there
The originally approved condition report was apparently rejected and replaced with a
    would be inadequate flow to certain safety related components under design basis
new evaluation and new corrective actions on March 30, 2003. The new evaluation
    conditions. The new evaluation also concluded that the setpoint was adequate if a
documented a vendor calculation which showed that with the 50 psig setpoint, there
    failure of the non-seismically qualified discharge piping did not have to be postulated
would be inadequate flow to certain safety related components under design basis
    during a loss of coolant event. Relying upon this latter conclusion, the licensee
conditions. The new evaluation also concluded that the setpoint was adequate if a
    determined that the 50 psig setpoint was acceptable. The team did not agree with the
failure of the non-seismically qualified discharge piping did not have to be postulated
    licensees reliance on non-seismically qualified piping to ensure that safety related
during a loss of coolant event. Relying upon this latter conclusion, the licensee
    components had adequate flow. Therefore, the team determined that the revised
determined that the 50 psig setpoint was acceptable. The team did not agree with the
    evaluation still did not address the SSDI violation in that the calculational basis for the
licensees reliance on non-seismically qualified piping to ensure that safety related
    50 psig issue still did not exist.
components had adequate flow. Therefore, the team determined that the revised
    The team noted that the evaluation contained in the revised CR 02-07802 was similar to
evaluation still did not address the SSDI violation in that the calculational basis for the
    that documented in CR 02-05748. Both CRs articulated a view that, unless there was a
50 psig issue still did not exist.  
    seismic event, non-seismic lines did not have to be assumed to have failed. The team
The team noted that the evaluation contained in the revised CR 02-07802 was similar to
    questioned this premise, based on the information in 10 CFR Part 50, Appendix A,
that documented in CR 02-05748. Both CRs articulated a view that, unless there was a
    GDC. The team noted that the licensee had committed to following the draft version of
seismic event, non-seismic lines did not have to be assumed to have failed. The team
                                              56                                      Enclosure
questioned this premise, based on the information in 10 CFR Part 50, Appendix A,
GDC. The team noted that the licensee had committed to following the draft version of


these criteria, as documented in NUREG 0153, and committed to in the USAR. Draft
Enclosure
57
these criteria, as documented in NUREG 0153, and committed to in the USAR. Draft
General design criteria 2, in that NUREG, stated, in part, that components important to
General design criteria 2, in that NUREG, stated, in part, that components important to
safety were to be designed to withstand the effects of natural phenomena without loss
safety were to be designed to withstand the effects of natural phenomena without loss
of their safety function.
of their safety function.  
The team presented this information to the licensee engineers as part of the review of
The team presented this information to the licensee engineers as part of the review of
CR 02-05748. The engineers sought the advice of the regulatory assurance department
CR 02-05748. The engineers sought the advice of the regulatory assurance department
via CR 03-04018. The regulatory assurance department responded, in part, that, "It
via CR 03-04018. The regulatory assurance department responded, in part, that, "It
was not appropriate to apply the single failure criterion to non-safety systems,"
was not appropriate to apply the single failure criterion to non-safety systems,"
confirming the team position. The licensee then wrote a new CR (03-06507) and took
confirming the team position. The licensee then wrote a new CR (03-06507) and took
compensatory measures to close the SW discharge valve leading to the cooling tower.
compensatory measures to close the SW discharge valve leading to the cooling tower.  
The licensee also stated in CR 03-06507 that the issue involved application of single
The licensee also stated in CR 03-06507 that the issue involved application of single
failure assumptions for existing systems. The team noted that this appeared to be a
failure assumptions for existing systems. The team noted that this appeared to be a
continuation of the misunderstanding of application of design basis assumptions.
continuation of the misunderstanding of application of design basis assumptions.
Following the inspection, the licensee performed a PRA study on the likelihood of failure
Following the inspection, the licensee performed a PRA study on the likelihood of failure
of the non-safety-related piping and then applied the results of this analysis to justify the
of the non-safety-related piping and then applied the results of this analysis to justify the
issue described in CR 02-07802. As this analysis was performed significantly after the
issue described in CR 02-07802. As this analysis was performed significantly after the
end of the inspection, it was not reviewed by the team, and the team was not able to
end of the inspection, it was not reviewed by the team, and the team was not able to
evaluate the impact of this analysis on the licensing basis of the plant.
evaluate the impact of this analysis on the licensing basis of the plant.  
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to correct a previously identified violation of NRC requirements. Since
licensee failed to correct a previously identified violation of NRC requirements. Since
there was a performance deficiency, the team compared this performance deficiency to
there was a performance deficiency, the team compared this performance deficiency to
the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
Reactor Inspection Reports." The team concluded that the issue was more than minor
Reactor Inspection Reports." The team concluded that the issue was more than minor
because the licensee had not corrected a previous violation and was relying on
because the licensee had not corrected a previous violation and was relying on
non-safety-related equipment to perform a safety function under design bases
non-safety-related equipment to perform a safety function under design bases
conditions.
conditions.
The previously identified violation was evaluated in IR 05000346/2002014 as having
The previously identified violation was evaluated in IR 05000346/2002014 as having
very low safety significance (Green). This assessment has not changed. This finding
very low safety significance (Green). This assessment has not changed. This finding
was reviewed by Regional Management, in accordance with IMC 0612. The finding was
was reviewed by Regional Management, in accordance with IMC 0612. The finding was
determined to be of very low safety significance and concluded that the violation could
determined to be of very low safety significance and concluded that the violation could
be categorized as Green.
be categorized as Green.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
measures be established to assure that applicable regulatory requirements and the
measures be established to assure that applicable regulatory requirements and the
design basis were correctly translated into specifications, drawings, procedures, and
design basis were correctly translated into specifications, drawings, procedures, and
instructions. Furthermore, it requires that measures be provided for verifying or
instructions. Furthermore, it requires that measures be provided for verifying or
checking the adequacy of design, such as by the performance of design reviews, by the
checking the adequacy of design, such as by the performance of design reviews, by the
use of alternate or simplified calculational methods, or by the performance of a suitable
use of alternate or simplified calculational methods, or by the performance of a suitable
testing program.
testing program.
Contrary to the above, as of August 12, 2003, the licensee failed to verify that the
Contrary to the above, as of August 12, 2003, the licensee failed to verify that the
design of the SW system discharge path swapover setpoints were adequate.
design of the SW system discharge path swapover setpoints were adequate.  
Specifically, the analysis performed by the licensee showed that the established
Specifically, the analysis performed by the licensee showed that the established
setpoints were not adequate and the evaluation of the analysis accepted the inadequate
setpoints were not adequate and the evaluation of the analysis accepted the inadequate
setpoint based on non-safety-related equipment performing a safety-related function
setpoint based on non-safety-related equipment performing a safety-related function
                                          57                                      Enclosure


    under design basis conditions. Neither the analysis nor the evaluation corrected the
Enclosure
    non-conforming condition previously identified in IR 05000346/2002014.
58
    This is a violation of 10 CFR Part 50, Appendix B, Criterion III. The NRC Enforcement
under design basis conditions. Neither the analysis nor the evaluation corrected the
    Policy, Section VI.A.1, provides guidance on dispositioning of violations. Normally,
non-conforming condition previously identified in IR 05000346/2002014.
    violations of very low safety significance are not cited. However, the Enforcement Policy
This is a violation of 10 CFR Part 50, Appendix B, Criterion III. The NRC Enforcement
    notes four conditions under which an issued notice of violation with a reply will be
Policy, Section VI.A.1, provides guidance on dispositioning of violations. Normally,
    considered. The first of these conditions is, "The licensee failed to restore compliance
violations of very low safety significance are not cited. However, the Enforcement Policy
    within a reasonable time after a violation was identified." As the corrective action
notes four conditions under which an issued notice of violation with a reply will be
    generated in response to the NCV did not restore compliance, this condition has been
considered. The first of these conditions is, "The licensee failed to restore compliance
    met. (VIO 05000346/2003010-01)
within a reasonable time after a violation was identified." As the corrective action
.12 Service Water Discharge Check Valve Test Acceptance Criteria
generated in response to the NCV did not restore compliance, this condition has been
    Introduction: The team identified a violation of TS 4.05a an 10 CFR 50.55a, having very
met. (VIO 05000346/2003010-01)
    low safety significance. Specifically, the licensee failed to ensure that the service water
    .12 Service Water Discharge Check Valve Test Acceptance Criteria
    discharge check valve was tested in accordance with ASME Code. The primary cause
Introduction: The team identified a violation of TS 4.05a an 10 CFR 50.55a, having very
    of this violation was related to the cross-cutting areas of problem identification and
low safety significance. Specifically, the licensee failed to ensure that the service water
    resolution and human performance, because the licensee did not recognize that the
discharge check valve was tested in accordance with ASME Code. The primary cause
    corrective actions taken needed to ensure compliance with NRC requirements.
of this violation was related to the cross-cutting areas of problem identification and
    Description: The 2002 SSDI described a Green finding and NCV of 10 CFR Part 50,
resolution and human performance, because the licensee did not recognize that the
    Appendix B, Criterion XVI, regarding the licensees failure to adequately correct the SW
corrective actions taken needed to ensure compliance with NRC requirements.
    pump discharge check valve acceptance criteria. This was entered into the licensees
Description: The 2002 SSDI described a Green finding and NCV of 10 CFR Part 50,
    corrective action system as CR 02-07657. The team determined that the licensee
Appendix B, Criterion XVI, regarding the licensees failure to adequately correct the SW
    evaluated the concern in the NCV and determined that the valves were full open at flow
pump discharge check valve acceptance criteria. This was entered into the licensees
    rates greater than 7270 gpm. Therefore, the licensee concluded that no corrective
corrective action system as CR 02-07657. The team determined that the licensee
    actions to the procedure were necessary. The CR evaluation stated that CR 02-05784
evaluated the concern in the NCV and determined that the valves were full open at flow
    would address the differences in the stated flow rates in the USAR and system
rates greater than 7270 gpm. Therefore, the licensee concluded that no corrective
    description. No formal calculation was prepared to support the 7270 gpm value and no
actions to the procedure were necessary. The CR evaluation stated that CR 02-05784
    corrective actions were generated for the CR. This CR was accepted as being ready for
would address the differences in the stated flow rates in the USAR and system
    closure on January 28, 2003.
description. No formal calculation was prepared to support the 7270 gpm value and no
    The team noted the licensees evaluation of the flow rate at which the valves were full
corrective actions were generated for the CR. This CR was accepted as being ready for
    open could not be reproduced as it relied on oral information provided by the valve
closure on January 28, 2003.
    vendor. The team identified that numerous check valve failures had been identified in
The team noted the licensees evaluation of the flow rate at which the valves were full
    the industry which were not detected during inservice testing of check valves to values
open could not be reproduced as it relied on oral information provided by the valve
    less than the required accident flow rate. Furthermore, the evaluation did not follow any
vendor. The team identified that numerous check valve failures had been identified in
    of the methods listed in GL 89-04, "Guidance on Developing Acceptable Inservice
the industry which were not detected during inservice testing of check valves to values
    Testing Programs" or NUREG 1482, "Guidelines for Inservice Testing Programs at
less than the required accident flow rate. Furthermore, the evaluation did not follow any
    Nuclear Power Plants" for ensuring that the valves were full open.
of the methods listed in GL 89-04, "Guidance on Developing Acceptable Inservice
    The team reviewed the licensees technical specification 4.05a and confirmed that the
Testing Programs" or NUREG 1482, "Guidelines for Inservice Testing Programs at
    licensee was required to test their check valves in accordance with the ASME Code for
Nuclear Power Plants" for ensuring that the valves were full open.
    Operation and Maintenance of Nuclear Power Plants (ASME OM Code) as required by
The team reviewed the licensees technical specification 4.05a and confirmed that the
    10 CFR 50.55a. The team confirmed that the licensee was committed to the 1996
licensee was required to test their check valves in accordance with the ASME Code for
    Addenda of the OM Code. Section ISTC 4.5.4a of this addenda stated that check
Operation and Maintenance of Nuclear Power Plants (ASME OM Code) as required by
    valves which had a safety function to open were to be tested by initiating flow and
10 CFR 50.55a. The team confirmed that the licensee was committed to the 1996
    observing that the valve had traveled to the full open position or to the position required
Addenda of the OM Code. Section ISTC 4.5.4a of this addenda stated that check
                                              58                                      Enclosure
valves which had a safety function to open were to be tested by initiating flow and
observing that the valve had traveled to the full open position or to the position required


to perform its intended function. Using the guidance in GL 89-04, the team ascertained
Enclosure
59
to perform its intended function. Using the guidance in GL 89-04, the team ascertained
that "the position required to perform its intended function" would be one which passed
that "the position required to perform its intended function" would be one which passed
the required accident flow rate.
the required accident flow rate.  
The team noted that the GL provided guidance for cases where a full flow test on a
The team noted that the GL provided guidance for cases where a full flow test on a
check valve could not be performed. For these cases, the licensee should submit a
check valve could not be performed. For these cases, the licensee should submit a
relief request from the ASME requirements to the NRC and have the request granted
relief request from the ASME requirements to the NRC and have the request granted
prior to implementing the requested relief.
prior to implementing the requested relief.
Based on the above, the team concluded that the licensees evaluation in CR 02-07657
Based on the above, the team concluded that the licensees evaluation in CR 02-07657
was inadequate in it did not demonstrate that 7270 gpm flow would ensure that the
was inadequate in it did not demonstrate that 7270 gpm flow would ensure that the
check valve was in the full open position. Because of this inadequate evaluation, the
check valve was in the full open position. Because of this inadequate evaluation, the
licensee did not take appropriate corrective actions to bring the surveillance procedure
licensee did not take appropriate corrective actions to bring the surveillance procedure
acceptance criteria into compliance with the requirements.
acceptance criteria into compliance with the requirements.
The team further reviewed CR 02-05784 and noted that it did not contain any references
The team further reviewed CR 02-05784 and noted that it did not contain any references
to CR 02-07657 and did not address the corrective actions which CR 02-05784 had
to CR 02-07657 and did not address the corrective actions which CR 02-05784 had
stated would be addressed by the CR. Specifically, there were no corrective actions
stated would be addressed by the CR. Specifically, there were no corrective actions
addressing the USAR and system description issues as stated by CR 02-07657.
addressing the USAR and system description issues as stated by CR 02-07657.  
Furthermore, the implementing organization had determined that the initially
Furthermore, the implementing organization had determined that the initially
recommended corrective actions to 02-05784 were not necessary and had
recommended corrective actions to 02-05784 were not necessary and had
recommended that they be canceled, although this recommendation had not been
recommended that they be canceled, although this recommendation had not been
formally accepted by the end of the inspection. The team ascertained that the accident
formally accepted by the end of the inspection. The team ascertained that the accident
analyses of record required a SW flow rate of approximately 10,300 gpm in order to
analyses of record required a SW flow rate of approximately 10,300 gpm in order to
ensure sufficient cooling of safety related systems.
ensure sufficient cooling of safety related systems.
Following the on-site inspection, the team performed a limited review of CR 03-07656.
Following the on-site inspection, the team performed a limited review of CR 03-07656.  
This CR noted that the SW pump #3 discharge check valve had not met the
This CR noted that the SW pump #3 discharge check valve had not met the
procedurally required acceptance criteria. The operability evaluation for this CR
procedurally required acceptance criteria. The operability evaluation for this CR
accepted the deficiency as operable based on the inadequate evaluation in CR 02-
accepted the deficiency as operable based on the inadequate evaluation in CR 02-
07657. Use of the evaluation from CR 02-07657 to justify operability resulted in the
07657. Use of the evaluation from CR 02-07657 to justify operability resulted in the
licensee using an alternate means of verifying that the check valve was full open without
licensee using an alternate means of verifying that the check valve was full open without
obtaining the necessary NRC approval for relief from the Code requirements.
obtaining the necessary NRC approval for relief from the Code requirements.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to demonstrate that the check valve could perform its intended function in
licensee failed to demonstrate that the check valve could perform its intended function in
accordance with NRC requirements. The team concluded that the issue was more than
accordance with NRC requirements. The team concluded that the issue was more than
minor because the inadequate test acceptance criteria allowed the licensee to accept a
minor because the inadequate test acceptance criteria allowed the licensee to accept a
check valve as performing its intended function at less than full system flow. The
check valve as performing its intended function at less than full system flow. The
licensee did not request NRC approval to use an alternate means of demonstrating the
licensee did not request NRC approval to use an alternate means of demonstrating the
valve was capable of performing its intended function. The team concluded that the
valve was capable of performing its intended function. The team concluded that the
issue involved traditional enforcement because the licensee had not sought NRC
issue involved traditional enforcement because the licensee had not sought NRC
approval prior to using an alternate means of demonstrating that a check valve could
approval prior to using an alternate means of demonstrating that a check valve could
perform its intended function.
perform its intended function.
In 2002, the issue was determined to be of very low safety significance. However,
In 2002, the issue was determined to be of very low safety significance. However,
because the licensee accepted a valve as being full open with less than the accident
because the licensee accepted a valve as being full open with less than the accident
required flow rate, the team re-evaluated the safety significance. The team determined
required flow rate, the team re-evaluated the safety significance. The team determined
that the licensee had an operability determination which concluded that the SW system
that the licensee had an operability determination which concluded that the SW system
                                          59                                    Enclosure


was operable but degraded, as it could not achieve design flow rates. This operability
Enclosure
60
was operable but degraded, as it could not achieve design flow rates. This operability
determination was reviewed by the resident inspectors and determined to be
determination was reviewed by the resident inspectors and determined to be
acceptable, as documented in IR 05000346/2003025. The team concluded that, as the
acceptable, as documented in IR 05000346/2003025. The team concluded that, as the
valve was part of the SW system, it was covered by this operability determination. As
valve was part of the SW system, it was covered by this operability determination. As
the licensee concluded the system was operable, the issue screened out of the Phase 1
the licensee concluded the system was operable, the issue screened out of the Phase 1
worksheet (Green).
worksheet (Green).
Line 3,143: Line 3,520:
inservice testing of valves in accordance with the ASME OM Code and applicable
inservice testing of valves in accordance with the ASME OM Code and applicable
addenda as required by 10 CFR 50, Section 50.55a.
addenda as required by 10 CFR 50, Section 50.55a.
Title 10 CFR 50.55a(f)(4) requires, in part, that, during successive 120 month intervals,
Title 10 CFR 50.55a(f)(4) requires, in part, that, during successive 120 month intervals,  
a licensee must comply with the requirements in the latest edition and addenda listed in
a licensee must comply with the requirements in the latest edition and addenda listed in
paragraph (b) of 10 CFR 50.55a 12 months prior to the start of the 120 month interval.
paragraph (b) of 10 CFR 50.55a 12 months prior to the start of the 120 month interval.  
Paragraph 50.55a(f)(5)(i) requires that the inservice test program be revised as
Paragraph 50.55a(f)(5)(i) requires that the inservice test program be revised as
necessary to meet the requirement of paragraph 50.55a(f)(4). Paragraph
necessary to meet the requirement of paragraph 50.55a(f)(4). Paragraph
50.55a(f)(5)(iii) requires that if a licensee determines that conformance with certain code
50.55a(f)(5)(iii) requires that if a licensee determines that conformance with certain code
requirements is impractical, the licensee is to submit information to support the
requirements is impractical, the licensee is to submit information to support the
Line 3,153: Line 3,530:
The ASME OM Code, 1996 addenda, Section ISTC 4.5.4(a) requires, in part, that check
The ASME OM Code, 1996 addenda, Section ISTC 4.5.4(a) requires, in part, that check
valves be exercised by initiating flow and observing that the obturator traveled to its full
valves be exercised by initiating flow and observing that the obturator traveled to its full
open position. The NRC approved use of the 1995 Code edition through the 1996
open position. The NRC approved use of the 1995 Code edition through the 1996
addenda for the third inservice testing 120-month interval on March 28, 2003 . Prior to
addenda for the third inservice testing 120-month interval on March 28, 2003 . Prior to
that date, the licensee was committed to the 1986 Edition (no Addenda) of the ASME
that date, the licensee was committed to the 1986 Edition (no Addenda) of the ASME
Boiler and Pressure Vessel Code, Section XI. The 1986 Code Edition contains similar
Boiler and Pressure Vessel Code, Section XI. The 1986 Code Edition contains similar
requirements.
requirements.
Contrary to the above, on September 12, 2003, and other dates, the licensee did not
Contrary to the above, on September 12, 2003, and other dates, the licensee did not
observe by a direct indicator or other positive means that the ASME Class 3 service
observe by a direct indicator or other positive means that the ASME Class 3 service
water pump discharge check valve obturator traveled to its full open position during its
water pump discharge check valve obturator traveled to its full open position during its
quarterly surveillance test. Specifically, on September 12, 2003, the licensee observed
quarterly surveillance test. Specifically, on September 12, 2003, the licensee observed
a flow rate of 9718 gpm through valve SW-19, which was less than the test acceptance
a flow rate of 9718 gpm through valve SW-19, which was less than the test acceptance
criterion of 10,000 gpm, and less than the approximately 10,300 gpm used in the
criterion of 10,000 gpm, and less than the approximately 10,300 gpm used in the
licensees most recent accident analysis. Observing flow rates less than required for the
licensees most recent accident analysis. Observing flow rates less than required for the
valve to perform its safety function was not a positive means to determine that the
valve to perform its safety function was not a positive means to determine that the
obturator traveled to its full open position and no other direct indicator or positive means
obturator traveled to its full open position and no other direct indicator or positive means
was used.
was used.
This is a violation of TS 4.05a and 10 CFR 50.55a. The NRC Enforcement Policy,
This is a violation of TS 4.05a and 10 CFR 50.55a. The NRC Enforcement Policy,
Section VI.A.1, provides guidance on dispositioning of violations. Normally, violations of
Section VI.A.1, provides guidance on dispositioning of violations. Normally, violations of
very low safety significance are not cited. However, the Enforcement Policy notes four
very low safety significance are not cited. However, the Enforcement Policy notes four
conditions under which an issued notice of violation with a reply will be considered. One
conditions under which an issued notice of violation with a reply will be considered. One
of these conditions is, "The licensee failed to restore compliance within a reasonable
of these conditions is, "The licensee failed to restore compliance within a reasonable
time after a violation was identified." As the CR addressing this issue was accepted for
time after a violation was identified." As the CR addressing this issue was accepted for
closure without restoring compliance by either revising the test acceptance criteria or
closure without restoring compliance by either revising the test acceptance criteria or
submitting a license amendment to the NRC to use an alternate means of verifying that
submitting a license amendment to the NRC to use an alternate means of verifying that
the valves were full open, this condition has been met. At the time of the exit, no new
the valves were full open, this condition has been met. At the time of the exit, no new
CR had been written to address this issue. (VIO 05000346/2003010-02)
CR had been written to address this issue. (VIO 05000346/2003010-02)
                                            60                                      Enclosure


.13 Lack of Design Basis Calculations to Support Service Water Single Failure
Enclosure
    Assumptions
61
    Introduction: The team identified an NCV of 10 CFR Part 50, Appendix B, Criterion III,
    .13 Lack of Design Basis Calculations to Support Service Water Single Failure
    having very low safety significance. Specifically, the licensee failed to provide an
Assumptions
    analysis which addressed the service water valve single failure assumptions mentioned
Introduction: The team identified an NCV of 10 CFR Part 50, Appendix B, Criterion III,
    in the updated safety analysis report. Following discovery, the licensee entered the
having very low safety significance. Specifically, the licensee failed to provide an
    issue in its corrective action program. The primary cause of this violation was related to
analysis which addressed the service water valve single failure assumptions mentioned
    the cross-cutting area of problem identification and resolution because the licensee had
in the updated safety analysis report. Following discovery, the licensee entered the
    not recognized the impact of the issue on the design basis and had not corrected it after
issue in its corrective action program. The primary cause of this violation was related to
    it was identified in 2002.
the cross-cutting area of problem identification and resolution because the licensee had
    Description: In IR 05000346/2002014, two URIs were identified dealing with the
not recognized the impact of the issue on the design basis and had not corrected it after
    ultimate heat sinks temperature and level analyses. A concern expressed in both URIs
it was identified in 2002.
    dealt with single failure assumptions of the SW discharge path valves to redirect flow in
Description: In IR 05000346/2002014, two URIs were identified dealing with the
    the most conservative manner. These single failure assumptions were described in the
ultimate heat sinks temperature and level analyses. A concern expressed in both URIs
    USAR as being the most limiting events for the SW system. For example, for the
dealt with single failure assumptions of the SW discharge path valves to redirect flow in
    maximum ultimate heat sink temperature case, a single failure of the forebay return
the most conservative manner. These single failure assumptions were described in the
    valve (SW 2930) to open would result in the SW discharge being directed approximately
USAR as being the most limiting events for the SW system. For example, for the
    17 feet from the intake, rather than some 500 feet away. This would increase the SW
maximum ultimate heat sink temperature case, a single failure of the forebay return
    temperature returning to the plant. For the minimum level case, a single failure of the
valve (SW 2930) to open would result in the SW discharge being directed approximately
    cooling water makeup valve (SW 2931) to close would result in water being diverted to
17 feet from the intake, rather than some 500 feet away. This would increase the SW
    the cooling towers instead of being returned to the ultimate heat sink, which would lower
temperature returning to the plant. For the minimum level case, a single failure of the
    the available level.
cooling water makeup valve (SW 2931) to close would result in water being diverted to
    Both valves were butterfly valves, and the licensee determined that the only credible
the cooling towers instead of being returned to the ultimate heat sink, which would lower
    failure was an electrical failure of the valve to change position. The licensee did have
the available level.
    procedures which addressed the operators opening (or closing) the valves manually as
Both valves were butterfly valves, and the licensee determined that the only credible
    needed. The team noted that the USAR stated that the operators needed to close the
failure was an electrical failure of the valve to change position. The licensee did have
    valves within three hours. However, the calculations for the ultimate heat sink maximum
procedures which addressed the operators opening (or closing) the valves manually as
    temperature and minimum water level started with the valves already opened (or
needed. The team noted that the USAR stated that the operators needed to close the
    closed). Because these calculations did not account for the three hour time delay, and
valves within three hours. However, the calculations for the ultimate heat sink maximum
    because the licensee did not have any calculation to support a different time period, the
temperature and minimum water level started with the valves already opened (or
    team considered them to be non-conservative in regard to both maximum temperature
closed). Because these calculations did not account for the three hour time delay, and
    and minimum level. As an interim measure the licensee implemented changes to
because the licensee did not have any calculation to support a different time period, the
    operations procedures to control the position of the valves to address the issue. The
team considered them to be non-conservative in regard to both maximum temperature
    licensee is also performing additional review and evaluations of the facilitys
and minimum level. As an interim measure the licensee implemented changes to
    conformance with design and licensing basis documents. The actions resolved any
operations procedures to control the position of the valves to address the issue. The
    immediate operability concerns regarding postulated single failures with maximum
licensee is also performing additional review and evaluations of the facilitys
    system temperatures and minimum heat sink level conditions.
conformance with design and licensing basis documents. The actions resolved any
    The ultimate heat sink calculations supported a change to the TSs (amendment 242). The
immediate operability concerns regarding postulated single failures with maximum
    team identified other problems with this submittal, as discussed in Section 4OA3(3)b.21.
system temperatures and minimum heat sink level conditions.
    Analysis: The team determined that a performance deficiency existed because the
The ultimate heat sink calculations supported a change to the TSs (amendment 242). The
    licensee failed to analyze the effects on the ultimate heat sink of the forebay return valve
team identified other problems with this submittal, as discussed in Section 4OA3(3)b.21.
    not opening or of the cooling water makeup valve not closing for the time period
Analysis: The team determined that a performance deficiency existed because the
    necessary for an operator to take action. Since there was a performance deficiency, the
licensee failed to analyze the effects on the ultimate heat sink of the forebay return valve
    team compared this performance deficiency to the minor questions contained in
not opening or of the cooling water makeup valve not closing for the time period
                                              61                                    Enclosure
necessary for an operator to take action. Since there was a performance deficiency, the
team compared this performance deficiency to the minor questions contained in


    Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The
Enclosure
    team concluded that the issue was more than minor because the current calculations
62
    were non-conservative and the licensee was not able to demonstrate that the SW
Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The
    system could perform its safety function under design basis conditions. This was a
team concluded that the issue was more than minor because the current calculations
    design issue which affected the mitigating systems cornerstone. The team determined
were non-conservative and the licensee was not able to demonstrate that the SW
    that it was unlikely that the SW system would not function during a design basis
system could perform its safety function under design basis conditions. This was a
    accident, as there would need to be the unlikely combination of both the "right" single
design issue which affected the mitigating systems cornerstone. The team determined
    failure along with the maximum temperature or minimum level conditions. The team
that it was unlikely that the SW system would not function during a design basis
    reviewed this finding in accordance with IMC 0609, "Significance Determination
accident, as there would need to be the unlikely combination of both the "right" single
    Process. The finding screened as Green in the SDP Phase 1, since this issue was a
failure along with the maximum temperature or minimum level conditions. The team
    design deficiency that would not likely result in the loss of function per Generic Letter
reviewed this finding in accordance with IMC 0609, "Significance Determination
    (GL) 91-18, Revision 1. Therefore, the issue was determined to have a very low safety
Process. The finding screened as Green in the SDP Phase 1, since this issue was a
    significance (Green).
design deficiency that would not likely result in the loss of function per Generic Letter
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
(GL) 91-18, Revision 1. Therefore, the issue was determined to have a very low safety
    measures be established to assure that applicable regulatory requirements and the
significance (Green).
    design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
    instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
    checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
    use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
    testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
    Contrary to the above, as of August 29, 2003, the ultimate heat sink maximum
use of alternate or simplified calculational methods, or by the performance of a suitable
    temperature and minimum level design basis, as described in the USAR had not been
testing program.
    correctly translated into a specification. Specifically, the USAR described a limiting
Contrary to the above, as of August 29, 2003, the ultimate heat sink maximum
    single failure for both the maximum temperature and minimum level condition, and the
temperature and minimum level design basis, as described in the USAR had not been
    design basis calculations did not address the time necessary for the operators to
correctly translated into a specification. Specifically, the USAR described a limiting
    recover from the single failure.
single failure for both the maximum temperature and minimum level condition, and the
    This issue was entered into the licensee's CAP as CRs 02-05372, 02-05986, 02-06337,
design basis calculations did not address the time necessary for the operators to
    03-06507, and 03-07042. Because this issue was of very low safety significance and
recover from the single failure.
    because it was entered into the licensees CAP, this violation is being treated as a NCV
This issue was entered into the licensee's CAP as CRs 02-05372, 02-05986, 02-06337,
    consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000346/2003010-17).
03-06507, and 03-07042. Because this issue was of very low safety significance and
.14 Auxiliary Feedwater System Calculation Issues With Main Steam Safety Valves
because it was entered into the licensees CAP, this violation is being treated as a NCV
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000346/2003010-17).
    having very low safety significance (Green). Specifically, the licensee failed to ensure
    .14 Auxiliary Feedwater System Calculation Issues With Main Steam Safety Valves
    that design analyses showed that the AFW system could perform its safety function
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    under design basis conditions. Following discovery, the licensee entered the issue into
having very low safety significance (Green). Specifically, the licensee failed to ensure
    its corrective action system. The primary cause of this violation was related to the
that design analyses showed that the AFW system could perform its safety function
    cross-cutting area of human performance, as the licensee used the results of a vendor
under design basis conditions. Following discovery, the licensee entered the issue into
    calculation without verifying that it was adequate.
its corrective action system. The primary cause of this violation was related to the
    Description: The team reviewed CR 02-07236 and the licensees calculation
cross-cutting area of human performance, as the licensee used the results of a vendor
    C-NSA-050.03-013 for AFW system hydraulic characteristics, which included calculating
calculation without verifying that it was adequate.
    the hydraulic resistance of flow to the steam generators. When determining the
Description: The team reviewed CR 02-07236 and the licensees calculation
    hydraulic system resistance, it was noted that the calculation did not consider the
C-NSA-050.03-013 for AFW system hydraulic characteristics, which included calculating
    increased backpressure caused by allowable MSSV drift and safety valve accumulation.
the hydraulic resistance of flow to the steam generators. When determining the
                                              62                                      Enclosure
hydraulic system resistance, it was noted that the calculation did not consider the
 
increased backpressure caused by allowable MSSV drift and safety valve accumulation.  
    This could have a negative affect on analyzed AFW pump flow because the higher
 
    backpressure would decrease AFW flow to the steam generators and reduce heat
Enclosure
    removal capability for the AFW system. In resolving this issue, the licensee reviewed
63
    the loss of feedwater analysis of record, 32-1171148-00, and determined that the MSSV
This could have a negative affect on analyzed AFW pump flow because the higher
    drift and accumulation had not been considered in this vendor calculation. The vendor
backpressure would decrease AFW flow to the steam generators and reduce heat
    calculation was used as an input to calculation C-NSA-050.03-013 for determining the
removal capability for the AFW system. In resolving this issue, the licensee reviewed
    AFW system resistance curve. Since the vendor calculation was in error, the licensees
the loss of feedwater analysis of record, 32-1171148-00, and determined that the MSSV
    calculation was in error as well.
drift and accumulation had not been considered in this vendor calculation. The vendor
    Analysis: The team determined that a performance deficiency existed because the
calculation was used as an input to calculation C-NSA-050.03-013 for determining the
    licensee failed to assess the effect of increased back pressure in the AFW system.
AFW system resistance curve. Since the vendor calculation was in error, the licensees
    Since there was a performance deficiency, the team compared this performance
calculation was in error as well.
    deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
Analysis: The team determined that a performance deficiency existed because the
    0612, "Power Reactor Inspection Reports." The team concluded that the issue was more
licensee failed to assess the effect of increased back pressure in the AFW system.  
    than minor because the calculations were non-conservative and because the calculation
Since there was a performance deficiency, the team compared this performance
    of record did not demonstrate that the AFW system could perform its safety function
deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
    under design basis conditions. Based on further analysis, the licensee concluded the
0612, "Power Reactor Inspection Reports." The team concluded that the issue was more
    AFW system was operable. This was a design issue which affected the mitigating
than minor because the calculations were non-conservative and because the calculation
    systems cornerstone. The team reviewed this finding in accordance with IMC 0609,
of record did not demonstrate that the AFW system could perform its safety function
    "Significance Determination Process, and answered no to all five screening questions
under design basis conditions. Based on further analysis, the licensee concluded the
    in the Phase 1 Screening Worksheet under the Mitigating Systems column. The team
AFW system was operable. This was a design issue which affected the mitigating
    concluded the issue was of very low safety significance (Green).
systems cornerstone. The team reviewed this finding in accordance with IMC 0609,
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
"Significance Determination Process, and answered no to all five screening questions
    measures be established to assure that applicable regulatory requirements and the
in the Phase 1 Screening Worksheet under the Mitigating Systems column. The team
    design basis were correctly translated into specifications, drawings, procedures, and
concluded the issue was of very low safety significance (Green).
    instructions. Furthermore, it requires that measures be provided for verifying or
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
    checking the adequacy of design, such as by the performance of design reviews, by the
measures be established to assure that applicable regulatory requirements and the
    use of alternate or simplified calculational methods, or by the performance of a suitable
design basis were correctly translated into specifications, drawings, procedures, and
    testing program.
instructions. Furthermore, it requires that measures be provided for verifying or
    Contrary to the above, the licensee failed to implement effective design control
checking the adequacy of design, such as by the performance of design reviews, by the
    measures to check and verify the adequacy of the design basis calculation performed by
use of alternate or simplified calculational methods, or by the performance of a suitable
    the vendor of the AFW system hydraulic analyses for all postulated accidents. This
testing program.
    issue negatively reflected on the adequacy of the licensees oversight of the engineering
Contrary to the above, the licensee failed to implement effective design control
    contractor performing the calculations. The licensee entered the issue into its CAP as
measures to check and verify the adequacy of the design basis calculation performed by
    CR 03-02651. Because this issue was of very low safety significance and because it
the vendor of the AFW system hydraulic analyses for all postulated accidents. This
    was entered into the licensees CAP, this violation is being treated as a NCV, consistent
issue negatively reflected on the adequacy of the licensees oversight of the engineering
    with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000346/2003010-18)
contractor performing the calculations. The licensee entered the issue into its CAP as
.15 Auxiliary Feedwater Strainer Mesh Size and Preconditioning of Auxiliary
CR 03-02651. Because this issue was of very low safety significance and because it
    Feedwater System During Testing
was entered into the licensees CAP, this violation is being treated as a NCV, consistent
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,
with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000346/2003010-18)
    having very low safety significance (Green). Specifically, the licensee failed to
    .15 Auxiliary Feedwater Strainer Mesh Size and Preconditioning of Auxiliary
    recognize that flushing the system and blowing down the strainers upstream of the
Feedwater System During Testing
    turbine driven pump bearing cooling water strainers prior to routine surveillances
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,
    constituted preconditioning of the AFW system. Following discovery, the licensee
having very low safety significance (Green). Specifically, the licensee failed to
    entered the preconditioning issue into the corrective action program. The primary cause
recognize that flushing the system and blowing down the strainers upstream of the
                                              63                                      Enclosure
turbine driven pump bearing cooling water strainers prior to routine surveillances
constituted preconditioning of the AFW system. Following discovery, the licensee
entered the preconditioning issue into the corrective action program. The primary cause


Enclosure
64
of this violation was related to the cross-cutting area of problem identification and
of this violation was related to the cross-cutting area of problem identification and
resolution, because the licensee had failed to recognize the consequences of the
resolution, because the licensee had failed to recognize the consequences of the
preconditioning when evaluating an earlier issue and determining that a larger mesh
preconditioning when evaluating an earlier issue and determining that a larger mesh
size could be installed in the strainers.
size could be installed in the strainers.
Description: The licensee designated CR 02-04673 as a SCAQ CR which described
Description: The licensee designated CR 02-04673 as a SCAQ CR which described
discovery that the strainers in the SW supply to the turbine driven pump bearings had a
discovery that the strainers in the SW supply to the turbine driven pump bearings had a
smaller mesh size than that of the main SW strainers. It also addressed the possibility
smaller mesh size than that of the main SW strainers. It also addressed the possibility
of blockage of the restricting orifices in the AFW system due to debris within the SW
of blockage of the restricting orifices in the AFW system due to debris within the SW
system. The following CRs were rolled into CR 02-04673: 02-05639 and 02-06861.
system. The following CRs were rolled into CR 02-04673: 02-05639 and 02-06861.  
Both an operability evaluation and a root cause report were required for CR 02-04673.
Both an operability evaluation and a root cause report were required for CR 02-04673.  
In addition, an engineering change package was initiated to add new strainers upstream
In addition, an engineering change package was initiated to add new strainers upstream
of the restricting orifices and to increase the mesh size in the existing strainers.
of the restricting orifices and to increase the mesh size in the existing strainers.
OPERABILITY DETERMINATION: Because the licensee had extensively cleaned the SW
OPERABILITY DETERMINATION: Because the licensee had extensively cleaned the SW
system piping during the outage, the team did not disagree with the conclusion reached
system piping during the outage, the team did not disagree with the conclusion reached
in the operability determination that the AFW system was operable. However, the
in the operability determination that the AFW system was operable. However, the
following non-conservatisms in the analysis were noted:
following non-conservatisms in the analysis were noted:
*       The operability determination assumed that the AFW system would run on
*
        minimum recirculation flow until all of the SW in the "dead leg" leading to the
The operability determination assumed that the AFW system would run on
        pumps has passed through the lines. However, under the postulated seismic
minimum recirculation flow until all of the SW in the "dead leg" leading to the
        event causing a loss of offsite power (LOOP), AFW would be required to function
pumps has passed through the lines. However, under the postulated seismic
        since the main feedwater pumps would be unavailable. The accident analysis
event causing a loss of offsite power (LOOP), AFW would be required to function
        assumed that AFW flow to the steam generators would be supplied within
since the main feedwater pumps would be unavailable. The accident analysis
        60 seconds. The starting sequence for the pumps would have the flow
assumed that AFW flow to the steam generators would be supplied within
        immediately being directed through the pumps and into the steam generators.
60 seconds. The starting sequence for the pumps would have the flow
        In the short term, 100 percent of the AFW flow would be directed into the steam
immediately being directed through the pumps and into the steam generators.  
        generators. Only after a period of time would the pumps be throttled back or the
In the short term, 100 percent of the AFW flow would be directed into the steam
        recirculation lines opened to divert water. Therefore, the team did not agree that
generators. Only after a period of time would the pumps be throttled back or the
        this assumption was reasonable. Furthermore, it appeared that the licensees
recirculation lines opened to divert water. Therefore, the team did not agree that
        analysis had not considered the actual design basis for the system.
this assumption was reasonable. Furthermore, it appeared that the licensees
*       The operability determination noted that the bearing strainers had not shown any
analysis had not considered the actual design basis for the system.
        sign of clogging during periodic testing with SW. However, the licensee failed to
*
        note that this was because the procedures required the line to be flushed and
The operability determination noted that the bearing strainers had not shown any
        the strainers to be blown down prior to and after each test, thus eliminating the
sign of clogging during periodic testing with SW. However, the licensee failed to
        potential for any clogging.
note that this was because the procedures required the line to be flushed and
ROOT CAUSE REPORT: The licensee issued a root cause analysis in March 2003 which
the strainers to be blown down prior to and after each test, thus eliminating the
determined the cause of the limiting particle size for the AFW strainers. At that time, the
potential for any clogging.
licensee's CAP did not require use of a formal root cause process. Therefore, even
ROOT CAUSE REPORT: The licensee issued a root cause analysis in March 2003 which  
determined the cause of the limiting particle size for the AFW strainers. At that time, the
licensee's CAP did not require use of a formal root cause process. Therefore, even
though the issue was determined to be a SCAQ, the licensee did not determine the root
though the issue was determined to be a SCAQ, the licensee did not determine the root
cause because the issue was, as stated in the root cause report, "historical." The team
cause because the issue was, as stated in the root cause report, "historical." The team
ascertained that because the root cause report did not follow a formalized process, the
ascertained that because the root cause report did not follow a formalized process, the
report was actually more like an apparent cause analysis than a root cause evaluation.
report was actually more like an apparent cause analysis than a root cause evaluation.
Similar to the operability determination, the cause evaluation noted that the strainers to
Similar to the operability determination, the cause evaluation noted that the strainers to
the coolers were periodically flushed and blown down during testing. However, the
the coolers were periodically flushed and blown down during testing. However, the
                                          64                                      Enclosure


evaluation failed to recognize that this constituted preconditioning of the test. The report
Enclosure
65
evaluation failed to recognize that this constituted preconditioning of the test. The report
did not evaluate the beneficial impact that the pre-test flushing and strainer blowdown
did not evaluate the beneficial impact that the pre-test flushing and strainer blowdown
would have in regard to required maintenance of the coolers.
would have in regard to required maintenance of the coolers.
The modification history developed in the cause evaluation showed that the licensee
The modification history developed in the cause evaluation showed that the licensee
had significantly increased the strainer mesh sizes in 1985 without discussion of the
had significantly increased the strainer mesh sizes in 1985 without discussion of the
bearing oil cooler strainers. However, the evaluation did not address whether these
bearing oil cooler strainers. However, the evaluation did not address whether these
modifications resulted in changes to the testing procedures, such as the currently
modifications resulted in changes to the testing procedures, such as the currently
imposed pre and post test flushing and strainer blowdown.
imposed pre and post test flushing and strainer blowdown.
The evaluation did not address whether the cooler for the pump bearings could handle
The evaluation did not address whether the cooler for the pump bearings could handle
the increased particle size. There was no documentation in the evaluation which
the increased particle size. There was no documentation in the evaluation which
addressed the acceptability of the increased strainer mesh size on the components
addressed the acceptability of the increased strainer mesh size on the components
which the strainer was designed to protect. Although the evaluation discussed the need
which the strainer was designed to protect. Although the evaluation discussed the need
for operator attention to an alarm for a blocked strainer, it did not recognize that the
for operator attention to an alarm for a blocked strainer, it did not recognize that the
larger particles could cause blockage of a downstream component that could not be
larger particles could cause blockage of a downstream component that could not be
cleared by back-washing of the strainer.
cleared by back-washing of the strainer.
ENGINEERING CHANGE PACKAGE: The engineering change package, ECR 03-0074,
ENGINEERING CHANGE PACKAGE: The engineering change package, ECR 03-0074,
stated that a conceptual design was not necessary due to the simplicity of the design
stated that a conceptual design was not necessary due to the simplicity of the design
and the great deal of study that went into producing the initiation report. The package
and the great deal of study that went into producing the initiation report. The package
acknowledged that the strainers were in the lines which supply cooling water to the
acknowledged that the strainers were in the lines which supply cooling water to the
pump and turbine bearing oil coolers, the turbine governor oil cooler and the pump
pump and turbine bearing oil coolers, the turbine governor oil cooler and the pump
mechanical seals. However, it did not discuss why the increased strainer size would not
mechanical seals. However, it did not discuss why the increased strainer size would not
affect any of these components.
affect any of these components.
In response to the teams questions, the licensee provided the team with a vendor
In response to the teams questions, the licensee provided the team with a vendor
manual which contained a single line which stated that the bearing oil coolers had
manual which contained a single line which stated that the bearing oil coolers had
openings greater than 0.0625 inches such that they could handle the larger size
openings greater than 0.0625 inches such that they could handle the larger size
particles if the strainer mesh size was increased. The licensee engineers stated these
particles if the strainer mesh size was increased. The licensee engineers stated these
coolers were the limiting components. However, this information was not documented
coolers were the limiting components. However, this information was not documented
and there was no evidence that the licensee had considered this information prior to the
and there was no evidence that the licensee had considered this information prior to the
team's questions.
team's questions.
Further discussions with the licensee determined that the bearing oil coolers had never
Further discussions with the licensee determined that the bearing oil coolers had never
been opened for inspections and were not included in the GL 89-13 heat exchanger
been opened for inspections and were not included in the GL 89-13 heat exchanger
program. The team concluded this had not been a problem in the past because of the
program. The team concluded this had not been a problem in the past because of the
very small mesh strainer. The licensee wrote CR 03-06576 to address this issue.
very small mesh strainer. The licensee wrote CR 03-06576 to address this issue.  
Nonetheless, the team concluded that the modification was a work in progress as it had
Nonetheless, the team concluded that the modification was a work in progress as it had
not been implemented by the end of the inspection.
not been implemented by the end of the inspection.  
REVIEW OF PERIODIC TEST PROCEDURE: As discussed above, the issue of flushing the
REVIEW OF PERIODIC TEST PROCEDURE: As discussed above, the issue of flushing the
lines and blowing down the strainers both prior to and following a periodic surveillance
lines and blowing down the strainers both prior to and following a periodic surveillance
was reviewed by the team. This issue was raised based on a review of periodic
was reviewed by the team. This issue was raised based on a review of periodic
procedure DB-SP-04152, which used SW as the source of cooling water for the test
procedure DB-SP-04152, which used SW as the source of cooling water for the test
duration. The licensee investigated the issue and determined that other AFW
duration. The licensee investigated the issue and determined that other AFW
surveillance tests also flushed the lines and blew down the strainers prior to the test
surveillance tests also flushed the lines and blew down the strainers prior to the test
being performed. The team determined that the flushing of the lines blowing down of
being performed. The team determined that the flushing of the lines blowing down of
the strainers constituted pre-conditioning of the turbine driven AFW pumps because it
the strainers constituted pre-conditioning of the turbine driven AFW pumps because it
                                          65                                      Enclosure


    masked any performance problems which could occur during an actual event. The
Enclosure
    availability and reliability of the system was intended to be ensured through the periodic
66
    testing. The team noted that the licensee had stated that no problems with the strainers
masked any performance problems which could occur during an actual event. The
    had occurred as part of the justification for increasing the strainer mesh size. However,
availability and reliability of the system was intended to be ensured through the periodic
    the team concluded that the licensees procedural actions would have masked any
testing. The team noted that the licensee had stated that no problems with the strainers
    problems. A violation of NRC requirements was identified.
had occurred as part of the justification for increasing the strainer mesh size. However,
    Analysis: The team determined that a performance deficiency existed because the
the team concluded that the licensees procedural actions would have masked any
    licensees practice, as prescribed in site procedures, prevented the AFW system from
problems. A violation of NRC requirements was identified.
    being tested in its as-found condition. Since there was a performance deficiency, the
Analysis: The team determined that a performance deficiency existed because the
    team compared this performance deficiency to the minor questions contained in
licensees practice, as prescribed in site procedures, prevented the AFW system from
    Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The
being tested in its as-found condition. Since there was a performance deficiency, the
    team concluded that the issue was more than minor because there was not sufficient
team compared this performance deficiency to the minor questions contained in
    information to demonstrate that test requirements would have been met had the
Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The
    strainers not been blown down. This was a procedural issue which affected the
team concluded that the issue was more than minor because there was not sufficient
    mitigating systems cornerstone. Because the licensee's practices prevented a true
information to demonstrate that test requirements would have been met had the
    assessment of previous operability, the team could not determine if the turbine driven
strainers not been blown down. This was a procedural issue which affected the
    pumps would have been inoperable if the strainers were not blown down. However,
mitigating systems cornerstone. Because the licensee's practices prevented a true
    discussions with the licensee did not indicate that a large amount of material was seen
assessment of previous operability, the team could not determine if the turbine driven
    during the system flushes and strainer blowdowns. Therefore, the licensee considered
pumps would have been inoperable if the strainers were not blown down. However,
    the system to be operable. The team reviewed this finding in accordance with IMC
discussions with the licensee did not indicate that a large amount of material was seen
    0609, "Significance Determination Process, and answered no to all five screening
during the system flushes and strainer blowdowns. Therefore, the licensee considered
    questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.
the system to be operable. The team reviewed this finding in accordance with IMC
    The team concluded the issue was of very low safety significance (Green).
0609, "Significance Determination Process, and answered no to all five screening
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI requires, in part, that a test
questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.  
    program be established to demonstrate that components will perform satisfactorily in
The team concluded the issue was of very low safety significance (Green).
    service. Contrary to the above, as of September 29, 2003, the test procedures for the
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI requires, in part, that a test
    AFW turbine high speed stop and overspeed trip did not demonstrate that the system
program be established to demonstrate that components will perform satisfactorily in
    would perform satisfactorily in service because the test included a step to flush the
service. Contrary to the above, as of September 29, 2003, the test procedures for the
    cooling water lines and blow down the strainers prior to performing the test. These
AFW turbine high speed stop and overspeed trip did not demonstrate that the system
    actions prevented any adverse effects due to strainer blockage from being discovered.
would perform satisfactorily in service because the test included a step to flush the
    Failure to adequately test the system was a violation of Appendix B, Criterion XI. This
cooling water lines and blow down the strainers prior to performing the test. These
    issue has been entered into the licensee's CAP as CR 03-06520. This violation is being
actions prevented any adverse effects due to strainer blockage from being discovered.  
    treated as a NCV consistent with Section VI.A.1 of the NRC Enforcement Policy.
Failure to adequately test the system was a violation of Appendix B, Criterion XI. This
    (NCV 05000346/2003010-19)
issue has been entered into the licensee's CAP as CR 03-06520. This violation is being
.16 Inadequate Evaluation of System Health Condition Report on Auxiliary Feedwater
treated as a NCV consistent with Section VI.A.1 of the NRC Enforcement Policy.
    Design Bases Calculations
(NCV 05000346/2003010-19)
    Introduction: The team identified a performance deficiency involving the licensee's
    .16 Inadequate Evaluation of System Health Condition Report on Auxiliary Feedwater
    failure to adequately evaluate a condition report written as part of the licensee's internal
Design Bases Calculations
    system health assessment. Following discovery, the licensee made corrections to the
Introduction: The team identified a performance deficiency involving the licensee's
    existing condition report evaluation. This was a minor violation.
failure to adequately evaluate a condition report written as part of the licensee's internal
    Description: During review of CR 02-05904, the team identified that the cause
system health assessment. Following discovery, the licensee made corrections to the
    evaluation was not adequately performed. This CR addressed a system health report
existing condition report evaluation. This was a minor violation.
    issue on whether certain AFW design basis calculations existed or were outdated. The
Description: During review of CR 02-05904, the team identified that the cause
                                              66                                    Enclosure
evaluation was not adequately performed. This CR addressed a system health report
issue on whether certain AFW design basis calculations existed or were outdated. The


    evaluation determined that all the questioned calculations did exist and that no further
Enclosure
    action was needed. The following deficiencies in the evaluation were identified:
67
    *       The evaluation listed an incorrect calculation number and an incorrect revision
evaluation determined that all the questioned calculations did exist and that no further
            for another calculation.
action was needed. The following deficiencies in the evaluation were identified:
    *       The evaluation identified a calculation for maximum steam pressure in the AFW
*
            system; however, it failed to recognize that the calculation was incorrect (this
The evaluation listed an incorrect calculation number and an incorrect revision
            issue is discussed in Section 4OA3(3)b.14).
for another calculation.
    *       The evaluation stated that CR 02-06356 identified the causes for the condition;
*
            therefore, no additional action needed to be taken. However, CR 02-06356,
The evaluation identified a calculation for maximum steam pressure in the AFW
            which had been evaluated three months prior to CR 02-05904, did not actually
system; however, it failed to recognize that the calculation was incorrect (this
            identify the causes, but rather assumed that the causes were known and that all
issue is discussed in Section 4OA3(3)b.14).
            appropriate corrective actions had been identified (this issue is discussed in
*
            Section 4OA3(3)b.22).
The evaluation stated that CR 02-06356 identified the causes for the condition;
    Analysis: The team determined that a performance deficiency existed because the
therefore, no additional action needed to be taken. However, CR 02-06356,
    licensee failed to evaluate a condition adverse to quality regarding calculations on the
which had been evaluated three months prior to CR 02-05904, did not actually
    AFW system. Since there was a performance deficiency, the team compared this
identify the causes, but rather assumed that the causes were known and that all
    performance deficiency to the minor questions contained in Appendix B, "Issue
appropriate corrective actions had been identified (this issue is discussed in
    Screening," of IMC 0612, "Power Reactor Inspection Reports." Because the team
Section 4OA3(3)b.22).
    independently identified the deficiencies which the licensee had failed to assess, the
Analysis: The team determined that a performance deficiency existed because the
    failure to properly evaluate an identified condition adverse to quality had no safety
licensee failed to evaluate a condition adverse to quality regarding calculations on the
    impact. Therefore, the team concluded this performance deficiency was minor.
AFW system. Since there was a performance deficiency, the team compared this
    Enforcement: The failure to perform an adequate cause evaluation for a condition
performance deficiency to the minor questions contained in Appendix B, "Issue
    adverse to quality constitutes a violation of 10 CFR Part 50, Appendix B, Criterion XVI,
Screening," of IMC 0612, "Power Reactor Inspection Reports." Because the team
    which has minor significance and is not subject to enforcement action in accordance with
independently identified the deficiencies which the licensee had failed to assess, the
    Section IV of the NRCs Enforcement Policy.
failure to properly evaluate an identified condition adverse to quality had no safety
    While minor violations are not normally documented in inspection reports, the team
impact. Therefore, the team concluded this performance deficiency was minor.
    determined that documentation was appropriate in this case due to the licensee's
Enforcement: The failure to perform an adequate cause evaluation for a condition
    inadequate evaluation. Additionally, the underlying cause is similar to that of other
adverse to quality constitutes a violation of 10 CFR Part 50, Appendix B, Criterion XVI,
    findings in this report.
which has minor significance and is not subject to enforcement action in accordance with
.17 Containment Post-LOCA Trisodium Phosphate
Section IV of the NRCs Enforcement Policy.
    Introduction: The team identified a performance deficiency involving the licensee failing
While minor violations are not normally documented in inspection reports, the team
    to approve a calculation prior to relying on the results of the calculation. The calculation
determined that documentation was appropriate in this case due to the licensee's
    addressed the capability of the TSP in baskets in the lower level of containment to
inadequate evaluation. Additionally, the underlying cause is similar to that of other
    control the pH of sump water following a postulated design basis accident. Following
findings in this report.
    discovery, the licensee entered the issue into its corrective action program and
    .17 Containment Post-LOCA Trisodium Phosphate
    approved and issued the calculation.
Introduction: The team identified a performance deficiency involving the licensee failing
    Description: The team reviewed CRs 02-02943, 02-05300 and 02-05304. These CRs
to approve a calculation prior to relying on the results of the calculation. The calculation
    questioned the adequacy of the TSP design from three aspects:
addressed the capability of the TSP in baskets in the lower level of containment to
                                              67                                      Enclosure
control the pH of sump water following a postulated design basis accident. Following
discovery, the licensee entered the issue into its corrective action program and
approved and issued the calculation.  
Description: The team reviewed CRs 02-02943, 02-05300 and 02-05304. These CRs
questioned the adequacy of the TSP design from three aspects:


*         Capability of the TSP baskets to perform their function in light of a new
Enclosure
          calculation for containment flood level which revealed that the baskets would not
68
          be fully submerged;
*
*         Two different calculations provided conflicting conclusion regarding the time
Capability of the TSP baskets to perform their function in light of a new
          when sump pH would be greater than 7.0; and
calculation for containment flood level which revealed that the baskets would not
*         Whether the amount of TSP in the baskets was sufficient to neutralize sump
be fully submerged;
          water with acidification from other post-LOCA sources such as degraded
*
          coatings and insulation.
Two different calculations provided conflicting conclusion regarding the time
when sump pH would be greater than 7.0; and
*
Whether the amount of TSP in the baskets was sufficient to neutralize sump
water with acidification from other post-LOCA sources such as degraded
coatings and insulation.
Concerns were also raised regarding the impact of the additional boric acid in the
Concerns were also raised regarding the impact of the additional boric acid in the
containment during the previous operating cycle on the capability of the TSP baskets to
containment during the previous operating cycle on the capability of the TSP baskets to
fulfill its safety function.
fulfill its safety function.
The licensee addressed the concerns of all three CRs through the corrective actions
The licensee addressed the concerns of all three CRs through the corrective actions
specified for CR 02-05300. Re-analysis of the containment flood level and the TSP
specified for CR 02-05300. Re-analysis of the containment flood level and the TSP
basket contents was performed in calculations C-NSA-059.01-019 and 86-5024418-01.
basket contents was performed in calculations C-NSA-059.01-019 and 86-5024418-01.  
These calculations demonstrated that, with the recalculated flood level, the amount of
These calculations demonstrated that, with the recalculated flood level, the amount of
TSP in the baskets was sufficient to meet the sump pH-control requirements of the
TSP in the baskets was sufficient to meet the sump pH-control requirements of the
USAR. Analysis of the impact of the additional boric acid inside the containment was
USAR. Analysis of the impact of the additional boric acid inside the containment was
performed in calculation C-NSA-040.01-006. This calculation evaluated the amount of
performed in calculation C-NSA-040.01-006. This calculation evaluated the amount of
TSP needed to neutralize the boric acid deposited in the containment from a variety of
TSP needed to neutralize the boric acid deposited in the containment from a variety of
RCS leakage scenarios, including RCS unidentified leakage over the previous three
RCS leakage scenarios, including RCS unidentified leakage over the previous three
operating cycles plus the boric acid deposited as the result of head leakage. This
operating cycles plus the boric acid deposited as the result of head leakage. This
calculation demonstrated that for the identified level of leakage, with the amount of boric
calculation demonstrated that for the identified level of leakage, with the amount of boric
acid deposited from the head leakage (conservatively assumed to be entirely dissolved
acid deposited from the head leakage (conservatively assumed to be entirely dissolved
into the sump), the TS required amount of TSP would neutralize all of the boric acid.
into the sump), the TS required amount of TSP would neutralize all of the boric acid.
The team found the issue difficult to evaluate as a result of the number of rollovers
The team found the issue difficult to evaluate as a result of the number of rollovers
involved in the resolution of these issues. The issues were ultimately consolidated into
involved in the resolution of these issues. The issues were ultimately consolidated into
three corrective actions under CR 02-05300; all three corrective actions involved the
three corrective actions under CR 02-05300; all three corrective actions involved the
completion of vendor calculation 86-5024418-01. The team determined that the three
completion of vendor calculation 86-5024418-01. The team determined that the three
corrective actions had been marked as completed although one calculation had not
corrective actions had been marked as completed although one calculation had not
been approved and had, in fact, been remanded to the vendor for revisions. This was
been approved and had, in fact, been remanded to the vendor for revisions. This was
not in accordance with the licensees CAP procedure. Specifically, procedure
not in accordance with the licensees CAP procedure. Specifically, procedure
NOP-LP-2001, Condition Report Process, Revisions 3 and 4, required that corrective
NOP-LP-2001, Condition Report Process, Revisions 3 and 4, required that corrective
actions be completed prior to the corrective action being accepted and closed. The
actions be completed prior to the corrective action being accepted and closed. The
revisions to the calculation were determined to be minor and did not affect the results,
revisions to the calculation were determined to be minor and did not affect the results,
and the licensee formally approved the calculation. The team did not review the final
and the licensee formally approved the calculation. The team did not review the final
calculation results.
calculation results.
The team determined that a performance deficiency existed because the issue involved
The team determined that a performance deficiency existed because the issue involved
the licensees failure to approve a calculation prior to relying on the results of the
the licensees failure to approve a calculation prior to relying on the results of the
calculation and this issue was not identified during the corrective action closure process.
calculation and this issue was not identified during the corrective action closure process.  
Since there was a performance deficiency, the team compared this performance
Since there was a performance deficiency, the team compared this performance
deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC
0612, "Power Reactor Inspection Reports." The team concluded that the performance
0612, "Power Reactor Inspection Reports." The team concluded that the performance
                                            68                                      Enclosure


    deficiency was minor because the changes to the unapproved calculation were minor
Enclosure
    and did not affect the overall results.
69
    Enforcement: The closure of all the corrective actions for CR 02-05300, contingent upon
deficiency was minor because the changes to the unapproved calculation were minor
    completion of vendor calculation 86-50244181-01, which had not been owner accepted,
and did not affect the overall results.
    was considered a violation of 10 CFR Appendix B, Criterion V, which has minor
Enforcement: The closure of all the corrective actions for CR 02-05300, contingent upon
    significance and is not subject to enforcement action in accordance with Section IV of
completion of vendor calculation 86-50244181-01, which had not been owner accepted,
    the NRCs Enforcement Policy. The licensee entered the issue into its CAP as
was considered a violation of 10 CFR Appendix B, Criterion V, which has minor
    CR 03-07420.
significance and is not subject to enforcement action in accordance with Section IV of
    While minor violations are not normally documented in inspection reports, the team
the NRCs Enforcement Policy. The licensee entered the issue into its CAP as  
    determined that documentation was appropriate in this case due to the rollover issues
CR 03-07420.
    which were identified and the underlying cause is similar to that of other findings in this
While minor violations are not normally documented in inspection reports, the team
    report.
determined that documentation was appropriate in this case due to the rollover issues
.18 Borated Water Storage Tank Calculation Issues
which were identified and the underlying cause is similar to that of other findings in this
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
report.
    having very low safety significance. Specifically, the licensee failed to translate the
    .18 Borated Water Storage Tank Calculation Issues
    radiological consequences of leakage from engineered safety feature components
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    outside containment into calculations of record for post-accident control room dose and
having very low safety significance. Specifically, the licensee failed to translate the
    offsite boundary dose. Following discovery, the licensee entered the issue into its
radiological consequences of leakage from engineered safety feature components
    corrective action program and provided a bounding evaluation which demonstrated that
outside containment into calculations of record for post-accident control room dose and
    the increase in dose was within acceptable limits.
offsite boundary dose. Following discovery, the licensee entered the issue into its
    Description: During the SSDI, the NRC identified that the radiological consequences of
corrective action program and provided a bounding evaluation which demonstrated that
    leakage from engineered safety features components outside the containment were not
the increase in dose was within acceptable limits.
    included in the calculation of offsite dose for 10 CFR Part 100 nor in the calculation for
Description: During the SSDI, the NRC identified that the radiological consequences of
    control room dose per GDC 19. The concerns involved the impact on control room dose
leakage from engineered safety features components outside the containment were not
    as a result of an airborne release from the assumed 500 gallons of containment sump
included in the calculation of offsite dose for 10 CFR Part 100 nor in the calculation for
    water deposited in the BWST and the impact on both offsite and control room dose as a
control room dose per GDC 19. The concerns involved the impact on control room dose
    result of ECCS system pump seal leakage. The licensee wrote CRs 02-06701,
as a result of an airborne release from the assumed 500 gallons of containment sump
    02-07713, and 02-07701 to address these issues.
water deposited in the BWST and the impact on both offsite and control room dose as a
    The licensee performed an informal calculation in the cause analysis for CR 02-07701 to
result of ECCS system pump seal leakage. The licensee wrote CRs 02-06701,
    determine the increase in dose in the control room from the 500 gallons deposited in the
02-07713, and 02-07701 to address these issues.
    BWST. The calculation was based on the site boundary base dose listed in the USAR
The licensee performed an informal calculation in the cause analysis for CR 02-07701 to
    which resulted from the airborne release associated with the 500 gallons of post-LOCA
determine the increase in dose in the control room from the 500 gallons deposited in the
    water deposited in the BWST. This dose was determined by the Bechtel calculation of
BWST. The calculation was based on the site boundary base dose listed in the USAR
    record as 2.72 rem. Using control room ventilation system parameters and the site
which resulted from the airborne release associated with the 500 gallons of post-LOCA
    boundary dose, the control room dose was calculated as 0.07 rem. The licensee
water deposited in the BWST. This dose was determined by the Bechtel calculation of
    extrapolated the dose for the 40 gallon per hour pump seal leakage from the USAR
record as 2.72 rem. Using control room ventilation system parameters and the site
    dose rate for normal valve system leakage of 5890 cubic centimeters per hour (1.56
boundary dose, the control room dose was calculated as 0.07 rem. The licensee
    gallons per hour). The result was an additional control room dose of 0.5 rem and an
extrapolated the dose for the 40 gallon per hour pump seal leakage from the USAR
    additional site boundary dose of 1.5 rem.
dose rate for normal valve system leakage of 5890 cubic centimeters per hour (1.56
    The licensee then calculated that the total offsite dose, resulting from the USAR value of
gallons per hour). The result was an additional control room dose of 0.5 rem and an
    232 rem accident dose plus the BWST dose of 2.72 rem plus the pump seal dose of
additional site boundary dose of 1.5 rem.
    1.5 rem, was a total of 236.22 rem. The total control room dose was similarly summed:
The licensee then calculated that the total offsite dose, resulting from the USAR value of
                                              69                                      Enclosure
232 rem accident dose plus the BWST dose of 2.72 rem plus the pump seal dose of
1.5 rem, was a total of 236.22 rem. The total control room dose was similarly summed:


Enclosure
70
USAR accident dose of 19.8 rem plus BWST dose of 0.066 rem plus pump seal leak
USAR accident dose of 19.8 rem plus BWST dose of 0.066 rem plus pump seal leak
dose of 0.5 rem for a total of 20.366 rem.
dose of 0.5 rem for a total of 20.366 rem.
As a result of these calculations, the licensee specified post-restart corrective actions to
As a result of these calculations, the licensee specified post-restart corrective actions to
update the Bechtel calculation of record and the USAR to incorporate these doses.
update the Bechtel calculation of record and the USAR to incorporate these doses.  
Because the corrective actions had not yet been completed, the licensee had not
Because the corrective actions had not yet been completed, the licensee had not
completed a screening or evaluation under 10 CFR 50.59. The team performed a
completed a screening or evaluation under 10 CFR 50.59. The team performed a
limited evaluation of the acceptability of the increased dose under 10 CFR
limited evaluation of the acceptability of the increased dose under 10 CFR
50.59(c)(2)(iii), "Result in more than a minimal increase in the consequences of an
50.59(c)(2)(iii), "Result in more than a minimal increase in the consequences of an
accident previously evaluated in the final safety analysis report (as updated)." The team
accident previously evaluated in the final safety analysis report (as updated)." The team
reviewed the guidance provided in Nuclear Energy Institute (NEI) standard 96-07,
reviewed the guidance provided in Nuclear Energy Institute (NEI) standard 96-07,
"Guidelines for 10 CFR 50.59 Implementation," Revision 1, which NRC endorsed in
"Guidelines for 10 CFR 50.59 Implementation," Revision 1, which NRC endorsed in
Line 3,594: Line 3,989:
Based on this guidance, the team determined the revised dose calculations did not
Based on this guidance, the team determined the revised dose calculations did not
result in more than a minimal increase in the consequences of an accident previously
result in more than a minimal increase in the consequences of an accident previously
evaluated in the USAR. The team determined that a more than minimal increase would
evaluated in the USAR. The team determined that a more than minimal increase would
have occurred if:
have occurred if:
*       The increase in dose was more than or equal to ten percent of the difference
*
        between the previously calculated dose value and the regulatory guideline value
The increase in dose was more than or equal to ten percent of the difference
        (10 CFR Part 100 or GDC 19); and
between the previously calculated dose value and the regulatory guideline value
*       The increased dose exceeded the current standard review plan guideline value
(10 CFR Part 100 or GDC 19); and
        for the particular design basis event.
*
The increased dose exceeded the current standard review plan guideline value
for the particular design basis event.
The team calculated that ten percent of the difference between the previously calculated
The team calculated that ten percent of the difference between the previously calculated
dose total and the 10 CFR Part 100 and GDC 19 limits were 6.8 rem for the offsite dose
dose total and the 10 CFR Part 100 and GDC 19 limits were 6.8 rem for the offsite dose
increase and 1.02 rem for the control room dose. The team confirmed that the total
increase and 1.02 rem for the control room dose. The team confirmed that the total
increases in dose of 4.2 and 0.57 rem were below the guidance values in NEI 96-07;
increases in dose of 4.2 and 0.57 rem were below the guidance values in NEI 96-07;
therefore, the first part of the guidance was satisfied. The team concluded that the
therefore, the first part of the guidance was satisfied. The team concluded that the
second part of the guidance was met because the total offsite dose was less than the
second part of the guidance was met because the total offsite dose was less than the
Part 100 limit of 300 rem and the control room dose was less than the GDC 19 limit of
Part 100 limit of 300 rem and the control room dose was less than the GDC 19 limit of
30 rem. The team, therefore, deemed that the licensee had an acceptable rationale for
30 rem. The team, therefore, deemed that the licensee had an acceptable rationale for
delaying issuance of the formal calculations until after restart.
delaying issuance of the formal calculations until after restart.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee had not recognized that the radiological consequences of leakage from
licensee had not recognized that the radiological consequences of leakage from
engineered safety features components outside the containment were not included in
engineered safety features components outside the containment were not included in
the calculation of offsite dose for 10 CFR Part 100 nor in the calculation for control room
the calculation of offsite dose for 10 CFR Part 100 nor in the calculation for control room
dose per GDC 19. Since there was a performance deficiency, the team compared this
dose per GDC 19. Since there was a performance deficiency, the team compared this
performance deficiency to the minor questions contained in Appendix B, "Issue
performance deficiency to the minor questions contained in Appendix B, "Issue
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
that the issue was more than minor because the licensee had to perform calculations to
that the issue was more than minor because the licensee had to perform calculations to
show that the increased doses remained within the post accident dose level
show that the increased doses remained within the post accident dose level
Line 3,622: Line 4,019:
The team reviewed the SDP questions for reactor safety, occupation radiation safety
The team reviewed the SDP questions for reactor safety, occupation radiation safety
and public radiation safety contained in MC 0612, Appendix B, Issue Screening, and
and public radiation safety contained in MC 0612, Appendix B, Issue Screening, and
                                          70                                      Enclosure


    also consulted with the senior reactor analysts (SRAs). Based on this review, the team
Enclosure
    determined that the issue was not covered by any of the revised oversight cornerstones
71
    and was, therefore, not suitable for SDP analysis. This determination was based on the
also consulted with the senior reactor analysts (SRAs). Based on this review, the team
    issue being a design issue that dealt with postulated doses following a design basis
determined that the issue was not covered by any of the revised oversight cornerstones
    accident. The team also determined that the increase in dose did not involve an issue
and was, therefore, not suitable for SDP analysis. This determination was based on the
    requiring a license amendment. Therefore, this finding was reviewed by Regional
issue being a design issue that dealt with postulated doses following a design basis
    Management, in accordance with IMC 0612. The finding was determined to be of very
accident. The team also determined that the increase in dose did not involve an issue
    low safety significance (Green) because the preliminary calculations concluded that the
requiring a license amendment. Therefore, this finding was reviewed by Regional
    increased doses remained within the post accident dose level requirements and there
Management, in accordance with IMC 0612. The finding was determined to be of very
    were no actual releases.
low safety significance (Green) because the preliminary calculations concluded that the
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
increased doses remained within the post accident dose level requirements and there
    measures be established to assure that applicable regulatory requirements and the
were no actual releases.
    design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
    instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
    checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
    use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
    testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
    Contrary to the above, the licensee failed to translate the radiological consequences of
use of alternate or simplified calculational methods, or by the performance of a suitable
    leakage from engineered safety feature (ESF) components outside containment into
testing program.
    calculations of record for post-LOCA control room dose and offsite boundary dose.
Contrary to the above, the licensee failed to translate the radiological consequences of
    The licensee entered the issue into its CAP as CRs 02-06701, 02-07713, and 02-07701.
leakage from engineered safety feature (ESF) components outside containment into
    Because this violation was of very low safety significance and because it was entered
calculations of record for post-LOCA control room dose and offsite boundary dose.
    into the licensees CAP, this violation is being treated as a NCV consistent with
The licensee entered the issue into its CAP as CRs 02-06701, 02-07713, and 02-07701.  
    Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-20)
Because this violation was of very low safety significance and because it was entered
.19 Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover Stud
into the licensees CAP, this violation is being treated as a NCV consistent with
    Overstressing
Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-20)
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    .19 Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover Stud
    having very low safety significance. Specifically, the licensee failed to evaluate a
Overstressing
    potential overstressing condition on the reactor coolant pump casing-to-cover studs.
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    Following discovery, the licensee entered the issue into its corrective action program.
having very low safety significance. Specifically, the licensee failed to evaluate a
    The primary cause of this violation was related to the cross-cutting area of problem
potential overstressing condition on the reactor coolant pump casing-to-cover studs.  
    identification and resolution as the licensee closed a condition report without recognizing
Following discovery, the licensee entered the issue into its corrective action program.  
    that the apparent condition adverse to quality had not been addressed.
The primary cause of this violation was related to the cross-cutting area of problem
    Description: The team reviewed CR 02-08759. This CR questioned whether the RCP
identification and resolution as the licensee closed a condition report without recognizing
    casing-to-cover studs had been overstressed when the studs on all four pumps were
that the apparent condition adverse to quality had not been addressed.
    retensioned in 1996. The RCP casing-to-cover studs are part of the reactor coolant
Description: The team reviewed CR 02-08759. This CR questioned whether the RCP
    pressure boundary (RCPB).
casing-to-cover studs had been overstressed when the studs on all four pumps were
    The team identified the following deficiencies with the licensees handling of this CR:
retensioned in 1996. The RCP casing-to-cover studs are part of the reactor coolant
    *       The CR was closed based on a draft revision of a vendor calculation, SR-0964,
pressure boundary (RCPB).
            Revision 1, which was not accepted by the licensee until after the CR was
The team identified the following deficiencies with the licensees handling of this CR:
            closed.
*
                                              71                                      Enclosure
The CR was closed based on a draft revision of a vendor calculation, SR-0964,
Revision 1, which was not accepted by the licensee until after the CR was
closed.


*         The discrepant condition (possible overstressing of the studs) was neither
Enclosure
          analyzed as not being a concern nor field verified to not be a problem before the
72
          CR was closed. Instead the corrective action was canceled on the basis that the
*
          studs on pumps 1-1 and 1-2 had relaxed to within acceptable limits, therefore,
The discrepant condition (possible overstressing of the studs) was neither
          the studs on the other two pumps were also deemed acceptable.
analyzed as not being a concern nor field verified to not be a problem before the
*         The draft calculation only addressed the allowable stud tension for pumps 1-1
CR was closed. Instead the corrective action was canceled on the basis that the
          and 1-2, based on the new gaskets installed; it did not address the condition
studs on pumps 1-1 and 1-2 had relaxed to within acceptable limits, therefore,
          from 1996 for all four pumps or the continuing condition on pumps 2-1 and 2-2.
the studs on the other two pumps were also deemed acceptable.
*         When questioned by the NRC team the licensee had to go back to the vendor
*
          and obtain a new calculation to show that the previous stud elongation was
The draft calculation only addressed the allowable stud tension for pumps 1-1
          acceptable. However, no new CR was written to address the fact that 02-08759
and 1-2, based on the new gaskets installed; it did not address the condition
          had been closed without addressing the concern for which it had been written.
from 1996 for all four pumps or the continuing condition on pumps 2-1 and 2-2.
*         Instead of being provided with a new calculation, the vendor provided the
*
          licensee with a letter providing the maximum allowable stud elongation for the
When questioned by the NRC team the licensee had to go back to the vendor
          1996 configuration.
and obtain a new calculation to show that the previous stud elongation was
*         The actual 1996 as-left elongation values for some of the studs were greater
acceptable. However, no new CR was written to address the fact that 02-08759
          than the 24 mils specified in the vendor letter, although they were within the 26
had been closed without addressing the concern for which it had been written.
          mils specified in 1996. The licensee verbally evaluated the condition, but did not
*
          actually document the acceptability of the 1996 condition.
Instead of being provided with a new calculation, the vendor provided the
*         The vendor letter was appended to the CR file four months after the CR was
licensee with a letter providing the maximum allowable stud elongation for the
          closed and only after the team questioned why no CR was written about the
1996 configuration.
          issue.
*
The actual 1996 as-left elongation values for some of the studs were greater
than the 24 mils specified in the vendor letter, although they were within the 26
mils specified in 1996. The licensee verbally evaluated the condition, but did not
actually document the acceptability of the 1996 condition.
*
The vendor letter was appended to the CR file four months after the CR was
closed and only after the team questioned why no CR was written about the
issue.
Because of this sequence of events, the team performed a limited, independent
Because of this sequence of events, the team performed a limited, independent
verification of both the formal and informal calculation results, and then verified the
verification of both the formal and informal calculation results, and then verified the
actual installed stud elongation against the calculated allowable. The team determined
actual installed stud elongation against the calculated allowable. The team determined
that some studs were elongated to 25 mils; however, the quadrant average in all cases
that some studs were elongated to 25 mils; however, the quadrant average in all cases
was between 23.2 and 23.4 mils. The team determined that an average elongation of
was between 23.2 and 23.4 mils. The team determined that an average elongation of
24.3 mils would keep the stress levels below the maximum American Society of
24.3 mils would keep the stress levels below the maximum American Society of
Mechanical Engineers (ASME) boiler and pressure vessel code (the Code) allowable of
Mechanical Engineers (ASME) boiler and pressure vessel code (the Code) allowable of
23.6 kilo-pounds per square inch (ksi). Based on this independent evaluation, the team
23.6 kilo-pounds per square inch (ksi). Based on this independent evaluation, the team
concluded that the casing-to-cover studs on RCPs 2-1 and 2-2 were not overstressed
concluded that the casing-to-cover studs on RCPs 2-1 and 2-2 were not overstressed
and that none of the studs on any of the four RCPs not been overstressed in the past.
and that none of the studs on any of the four RCPs not been overstressed in the past.
The team also noted that the licensee did not have a design basis calculation that
The team also noted that the licensee did not have a design basis calculation that
supported the increased tensioning of the studs on all four reactor pumps in 1996 and
supported the increased tensioning of the studs on all four reactor pumps in 1996 and
still did not have such a calculation for RCPs 2-1 and 2-2 in 2003. However, the
still did not have such a calculation for RCPs 2-1 and 2-2 in 2003. However, the
licensee planned to replace the gaskets on these pumps by no later than RFO 14 in
licensee planned to replace the gaskets on these pumps by no later than RFO 14 in
2005; once the gaskets are replaced, the stud tensioning would be addressed by
2005; once the gaskets are replaced, the stud tensioning would be addressed by
calculation SR-0964.
calculation SR-0964.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to evaluate the acceptability of the RCP studs prior to closing the CR.
licensee failed to evaluate the acceptability of the RCP studs prior to closing the CR.  
Additionally, when the issue was brought to their attention, the licensee did not write a
Additionally, when the issue was brought to their attention, the licensee did not write a
                                            72                                      Enclosure


    new CR to document the failure of the CAP. Since there was a performance deficiency,
Enclosure
    the team compared this performance deficiency to the minor questions contained in
73
    Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The
new CR to document the failure of the CAP. Since there was a performance deficiency,
    team concluded that the issue was more than minor because the licensee had to
the team compared this performance deficiency to the minor questions contained in
    perform calculations to determine if the RCP studs were within ASME Code allowables.
Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The
    The team reviewed this finding in accordance with IMC 0609, "Significance
team concluded that the issue was more than minor because the licensee had to
    Determination Process. The team assessed the finding through Phase 1 of the SDP.
perform calculations to determine if the RCP studs were within ASME Code allowables.  
    The issue involved the barrier integrity cornerstone because it dealt with the
The team reviewed this finding in accordance with IMC 0609, "Significance
    acceptability of the RCPB. There was only one question related to the RCPB. The
Determination Process. The team assessed the finding through Phase 1 of the SDP.  
    licensee had not evaluated the functionality of RCP studs for past operation or for
The issue involved the barrier integrity cornerstone because it dealt with the
    current operation on two of the four pumps. Therefore, the team assessed the issue
acceptability of the RCPB. There was only one question related to the RCPB. The
    based on the team's evaluation described above. Based on this assessment, the RCP
licensee had not evaluated the functionality of RCP studs for past operation or for
    studs were always functional and the SDP RCPB question was answered as "no".
current operation on two of the four pumps. Therefore, the team assessed the issue
    Therefore, the finding screened out as having very low safety significance (Green).
based on the team's evaluation described above. Based on this assessment, the RCP
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
studs were always functional and the SDP RCPB question was answered as "no".  
    measures be established to assure that applicable regulatory requirements and the
Therefore, the finding screened out as having very low safety significance (Green).
    design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
    instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
    checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
    use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
    testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
    Contrary to the above, in March 2003, the licensee closed CR 02-08759 without
use of alternate or simplified calculational methods, or by the performance of a suitable
    ensuring that the ASME Code requirements were correctly translated into the torquing
testing program.
    values for the RCP casing-to-cover studs and without ensuring that previous
Contrary to the above, in March 2003, the licensee closed CR 02-08759 without
    maintenance activities had not resulted in the studs being overstressed.
ensuring that the ASME Code requirements were correctly translated into the torquing
    After being identified as a potential violation at the end of the inspection, the licensee
values for the RCP casing-to-cover studs and without ensuring that previous
    wrote CR 03-07047 to enter the issue into the CAP. Since the issue was of very low
maintenance activities had not resulted in the studs being overstressed.
    safety significance and was captured in the licensee's CAP, it is being treated as a NCV,
After being identified as a potential violation at the end of the inspection, the licensee
    consistent with Section VI.A.1 of the NRC Enforcement Policy.
wrote CR 03-07047 to enter the issue into the CAP. Since the issue was of very low
    (NCV 05000346/2003010-21)
safety significance and was captured in the licensee's CAP, it is being treated as a NCV,
.20 Reactor Coolant Pump Inner Gasket Leakage
consistent with Section VI.A.1 of the NRC Enforcement Policy.  
    The team reviewed CRs 02-01523, 02-03668, and 03-04018, and associated
(NCV 05000346/2003010-21)
    evaluations, which documented an apparent continuing problem with RCP inner gasket
    .20 Reactor Coolant Pump Inner Gasket Leakage
    leakage. The team determined that the licensee failed to adequately analyze the results
The team reviewed CRs 02-01523, 02-03668, and 03-04018, and associated
    of an apparent continuing leak past the inner gasket on the RCPs. Specifically, minor
evaluations, which documented an apparent continuing problem with RCP inner gasket
    leakage past the inner gasket was noted on all four pumps during previous outages and
leakage. The team determined that the licensee failed to adequately analyze the results
    the documented evaluation did not address why it was acceptable to not repair the
of an apparent continuing leak past the inner gasket on the RCPs. Specifically, minor
    gaskets. Furthermore, the licensee's analysis did not provide technical justification for
leakage past the inner gasket was noted on all four pumps during previous outages and
    either replacing or not replacing all four RCP gaskets.
the documented evaluation did not address why it was acceptable to not repair the
    The team performed extensive evaluation of the as-left leakages for all pumps by
gaskets. Furthermore, the licensee's analysis did not provide technical justification for
    reviewing test results and test log books. The responsible test engineers were also
either replacing or not replacing all four RCP gaskets.
    interviewed by the team. The team determined that the licensees evaluations were
The team performed extensive evaluation of the as-left leakages for all pumps by
    based on leak testing that: (1) did not use the same methodology from outage to
reviewing test results and test log books. The responsible test engineers were also
                                              73                                        Enclosure
interviewed by the team. The team determined that the licensees evaluations were
based on leak testing that: (1) did not use the same methodology from outage to


    outage; (2) did not attempt to normalize the data from outage to outage; (3) did not
Enclosure
    consider the impact of reactor coolant pressure and temperature conditions on the test
74
    results; and (4) was only intended to verify that the leak detection lines were open and
outage; (2) did not attempt to normalize the data from outage to outage; (3) did not
    not blocked. The team was concerned that the licensee did not recognize these
consider the impact of reactor coolant pressure and temperature conditions on the test
    inconsistencies in performing and approving the evaluation.
results; and (4) was only intended to verify that the leak detection lines were open and
    The team determined that the design of both the inner and outer gaskets was to seal
not blocked. The team was concerned that the licensee did not recognize these
    against full reactor pressure. While normally the inner gasket provided the seal, the
inconsistencies in performing and approving the evaluation.  
    outer gaskets was also designed for this purpose. Only if the outer gasket failed would
The team determined that the design of both the inner and outer gaskets was to seal
    the RCPB, provided by the casing-to-cover studs, be affected.
against full reactor pressure. While normally the inner gasket provided the seal, the
    The team also noted that leakage past either the inner or outer gasket was not pressure
outer gaskets was also designed for this purpose. Only if the outer gasket failed would
    boundary leakage, per the ASME Code. The Code specifically excluded gaskets from
the RCPB, provided by the casing-to-cover studs, be affected.
    RCPB leakage. Instead, any leakage past the outer gasket would be categorized as
The team also noted that leakage past either the inner or outer gasket was not pressure
    either identified or unidentified reactor coolant leakage, and would be subject to TS
boundary leakage, per the ASME Code. The Code specifically excluded gaskets from
    limits. Leakage past the inner gasket was not considered to be a safety concern.
RCPB leakage. Instead, any leakage past the outer gasket would be categorized as
    Neither the inner or the outer gasket was considered to be important to safety and
either identified or unidentified reactor coolant leakage, and would be subject to TS
    neither component was credited with having a safety function in the USAR.
limits. Leakage past the inner gasket was not considered to be a safety concern.  
    The team determined that a catastrophic failure of the inner gasket during an
Neither the inner or the outer gasket was considered to be important to safety and
    operational cycle should have no consequences, as the outer gasket should continue to
neither component was credited with having a safety function in the USAR.
    provide a seal. If the outer gasket also failed, then the licensee would have to comply
The team determined that a catastrophic failure of the inner gasket during an
    with the TS limiting conditions for operation and shut down the plant.
operational cycle should have no consequences, as the outer gasket should continue to
    The team noted that the normal operating pressure and temperature (NOP/NOT) test
provide a seal. If the outer gasket also failed, then the licensee would have to comply
    performed by the licensee included inspections of the RCPs: both at the gasket leakoff
with the TS limiting conditions for operation and shut down the plant.
    lines and at the studs. These inspections were conducted prior to, during and following
The team noted that the normal operating pressure and temperature (NOP/NOT) test
    reaching NOP/NOT. This NOP/NOT test showed that there was no outer gasket
performed by the licensee included inspections of the RCPs: both at the gasket leakoff
    leakage and that the inner gasket leakage was minor, occurred primarily during the
lines and at the studs. These inspections were conducted prior to, during and following
    pressurization period and stopped, or significantly slowed, once the pumps reached an
reaching NOP/NOT. This NOP/NOT test showed that there was no outer gasket
    equilibrium temperature.
leakage and that the inner gasket leakage was minor, occurred primarily during the
    Notwithstanding that the licensee failed to adequately analyze the results of an apparent
pressurization period and stopped, or significantly slowed, once the pumps reached an
    continuing leak past the inner gasket on the RCPs, the team concluded that this did not
equilibrium temperature.
    present a safety issue since the inner gasket leakage would not affect the RCPB. No
Notwithstanding that the licensee failed to adequately analyze the results of an apparent
    violation of NRC requirements were identified.
continuing leak past the inner gasket on the RCPs, the team concluded that this did not
.21 Environmental Qualification of Equipment Not Supported by Analysis
present a safety issue since the inner gasket leakage would not affect the RCPB. No
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
violation of NRC requirements were identified.
    having very low safety significance (Green). Specifically, the licensee failed to ensure
    .21 Environmental Qualification of Equipment Not Supported by Analysis
    that emergency core cooling system pump motors were environmentally qualified for the
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
    stated mission time, as stated in a license amendment request (LAR) submitted to the
having very low safety significance (Green). Specifically, the licensee failed to ensure
    NRC. Following discovery, the licensee entered the issue into its corrective action
that emergency core cooling system pump motors were environmentally qualified for the
    program. The primary cause of this violation was related to the cross-cutting area of
stated mission time, as stated in a license amendment request (LAR) submitted to the
    human performance as the licensee did not ensure that personnel developing license
NRC. Following discovery, the licensee entered the issue into its corrective action
    documents had the necessary information.
program. The primary cause of this violation was related to the cross-cutting area of
                                              74                                    Enclosure
human performance as the licensee did not ensure that personnel developing license
documents had the necessary information.


Description: The team examined CR 02-05732, which was issued during the licensees
Enclosure
latent issues review of the SW system. The fundamental concern discussed in the CR
75
Description: The team examined CR 02-05732, which was issued during the licensees
latent issues review of the SW system. The fundamental concern discussed in the CR
was that LAR 96-0008, submitted to NRC by the licensee on July 28, 1999, contained
was that LAR 96-0008, submitted to NRC by the licensee on July 28, 1999, contained
statements that were unsupported by analyses.
statements that were unsupported by analyses.
The CR identified three specific concerns:
The CR identified three specific concerns:
*       Some equipment in the ECCS pump rooms was not qualified to higher
*
        temperatures, as stated in the request;
Some equipment in the ECCS pump rooms was not qualified to higher
*       There was no analysis to support a statement in the request that two room
temperatures, as stated in the request;
        coolers were adequate even with substantially degraded flow rates; and
*
*       The request stated that no changes were made in AFW flow, yet a calculation of
There was no analysis to support a statement in the request that two room
        record showed that the flow rate was changed from 1600 gpm to 800 gpm.
coolers were adequate even with substantially degraded flow rates; and
The team reviewed the condition description, immediate actions, and cause analysis.
*
The request stated that no changes were made in AFW flow, yet a calculation of
record showed that the flow rate was changed from 1600 gpm to 800 gpm.
The team reviewed the condition description, immediate actions, and cause analysis.  
The cause analysis examined the three concerns and concluded that there was no
The cause analysis examined the three concerns and concluded that there was no
discrepant condition, no apparent cause, and no corrective actions required.
discrepant condition, no apparent cause, and no corrective actions required.
The team disagreed with this conclusion based on a review of CR 02-05593 which
The team disagreed with this conclusion based on a review of CR 02-05593 which
identified a block of components that were not included in a calculation evaluating
identified a block of components that were not included in a calculation evaluating
environmental qualification (EQ) qualification of equipment in the ECCS pump rooms.
environmental qualification (EQ) qualification of equipment in the ECCS pump rooms.  
This CR also noted that no reference for qualification of the HPI and DHR pump motors
This CR also noted that no reference for qualification of the HPI and DHR pump motors
existed and recommended that the EQ calculation be revised to address qualification of
existed and recommended that the EQ calculation be revised to address qualification of
Line 3,820: Line 4,232:
of equipment in an ECCS pump room, the containment spray (CS) and HPI pump
of equipment in an ECCS pump room, the containment spray (CS) and HPI pump
motors, were not environmentally qualified for the service time of 30 days which was
motors, were not environmentally qualified for the service time of 30 days which was
stated in the LAR. Based on a review of the EQ folder, the team determined that the
stated in the LAR. Based on a review of the EQ folder, the team determined that the
motors could most likely be qualified as required. CR 03-06588 was written to address
motors could most likely be qualified as required. CR 03-06588 was written to address
this issue. However, the team later determined that the licensee had evaluated
this issue. However, the team later determined that the licensee had evaluated
CR 03-06588 and concluded that no corrective actions needed to be taken as far as
CR 03-06588 and concluded that no corrective actions needed to be taken as far as
environmentally qualifying the ECCS motors.
environmentally qualifying the ECCS motors.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
licensee failed to establish the environmental qualification of two ECCS motors at the
licensee failed to establish the environmental qualification of two ECCS motors at the
time the license amendment request was submitted. Since there was a performance
time the license amendment request was submitted. Since there was a performance
deficiency, the team compared this performance deficiency to the minor questions
deficiency, the team compared this performance deficiency to the minor questions
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
Reports." The team concluded that the failure to adequately evaluate the motor
Reports." The team concluded that the failure to adequately evaluate the motor
environmental qualification issue was more than minor because it reflected a weakness
environmental qualification issue was more than minor because it reflected a weakness
in the licensees CAP in regard to correctly assessing issues. The team concluded that,
in the licensees CAP in regard to correctly assessing issues. The team concluded that,
if uncorrected, this continuing weakness could result in a repeat failure of the CAP to
if uncorrected, this continuing weakness could result in a repeat failure of the CAP to
adequately identify, evaluate and correct problems. This was an equipment qualification
adequately identify, evaluate and correct problems. This was an equipment qualification
issue which affected the mitigating systems cornerstone. Although the licensee had not
issue which affected the mitigating systems cornerstone. Although the licensee had not
qualified the equipment, the team deemed that the motors more likely than not could be
qualified the equipment, the team deemed that the motors more likely than not could be
qualified. Therefore, the team considered it reasonable that the motors would perform
qualified. Therefore, the team considered it reasonable that the motors would perform
                                        75                                      Enclosure


    their safety function, if required to operate. The team reviewed this finding in
Enclosure
    accordance with IMC 0609, "Significance Determination Process. The finding was
76
    screened in the SDP Phase 1 as a qualification deficiency that was confirmed not to
their safety function, if required to operate. The team reviewed this finding in
    result in the loss of function per Generic Letter 91-18, Revision 1. Therefore, the issue
accordance with IMC 0609, "Significance Determination Process. The finding was
    was determined to have a very low safety significance (Green).
screened in the SDP Phase 1 as a qualification deficiency that was confirmed not to
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
result in the loss of function per Generic Letter 91-18, Revision 1. Therefore, the issue
    conditions adverse to quality be promptly identified and corrected, commensurate with
was determined to have a very low safety significance (Green).
    their safety significance.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
    Contrary to the above, in November 2003, the licensee evaluated CR 03-06588, which
conditions adverse to quality be promptly identified and corrected, commensurate with
    described a condition adverse to quality, and concluded that no corrective actions were
their safety significance.
    necessary. The condition adverse to quality described in the CR dealt with LAR 96-008
Contrary to the above, in November 2003, the licensee evaluated CR 03-06588, which
    which documented that the HPI and DHR pump motors were environmentally qualified
described a condition adverse to quality, and concluded that no corrective actions were
    for 30 days, when, in fact, those motors were not so qualified.
necessary. The condition adverse to quality described in the CR dealt with LAR 96-008
    After being identified as a potential violation at the end of the inspection, the licensee
which documented that the HPI and DHR pump motors were environmentally qualified
    wrote CR 03-06588 to enter the issue into the CAP. Since the issue was of very low
for 30 days, when, in fact, those motors were not so qualified.
    safety significance and was captured in the licensee's CAP, it is being treated as a NCV,
After being identified as a potential violation at the end of the inspection, the licensee
    consistent with Section VI.A.1 of the NRC Enforcement Policy.
wrote CR 03-06588 to enter the issue into the CAP. Since the issue was of very low
    (NCV 05000346/2003010-22)
safety significance and was captured in the licensee's CAP, it is being treated as a NCV,
.22 Inadequate Justification for Downgrade of Significant Condition Adverse to
consistent with Section VI.A.1 of the NRC Enforcement Policy.  
    Quality
(NCV 05000346/2003010-22)
    Introduction: The team identified a performance deficiency involving the licensee's
    .22 Inadequate Justification for Downgrade of Significant Condition Adverse to
    failure to evaluate an issue initially determined to be a significant condition adverse to
Quality
    quality prior to downgrading the issue. Following discovery, the licensee entered the
Introduction: The team identified a performance deficiency involving the licensee's
    issue into its corrective action program. This was a minor violation.
failure to evaluate an issue initially determined to be a significant condition adverse to
    Description: Prior to the safety system design inspection in October 2002, and following
quality prior to downgrading the issue. Following discovery, the licensee entered the
    completion of the system health reviews, the licensee initiated CR 02-06356 to
issue into its corrective action program. This was a minor violation.
    document a repetitive concern regarding a difficulty in determining the status or location
Description: Prior to the safety system design inspection in October 2002, and following
    of design basis calculations. This CR was determined to be a SCAQ, primarily because
completion of the system health reviews, the licensee initiated CR 02-06356 to
    a number of design basis calculations were discovered to be outdated or non-existent.
document a repetitive concern regarding a difficulty in determining the status or location
    Issues such as those discussed in Section 4OA3(3)b.16 exemplified the reason that the
of design basis calculations. This CR was determined to be a SCAQ, primarily because
    CR originally was rated as a significant condition.
a number of design basis calculations were discovered to be outdated or non-existent.
    The team reviewed CR 02-06356 and noted that it had been downgraded to a routine
Issues such as those discussed in Section 4OA3(3)b.16 exemplified the reason that the
    CR with minimal investigation or justification. The evaluator assumed that his
CR originally was rated as a significant condition.
    department had the bulk of the calculations and that he knew the status of those
The team reviewed CR 02-06356 and noted that it had been downgraded to a routine
    calculations. The evaluator then concluded that there was not really a problem, based
CR with minimal investigation or justification. The evaluator assumed that his
    on these assumptions and apparently without considering other design engineering
department had the bulk of the calculations and that he knew the status of those
    departments. Additionally, the team determined that the extent of condition review was
calculations. The evaluator then concluded that there was not really a problem, based
    based entirely on a word search for the word "calculation" in the title of CRs. This
on these assumptions and apparently without considering other design engineering
    eliminated many of the CRs written on superceded or historical calculations and resulted
departments. Additionally, the team determined that the extent of condition review was
    in many of the CRs on design basis calculational issues not being found.
based entirely on a word search for the word "calculation" in the title of CRs. This
                                              76                                        Enclosure
eliminated many of the CRs written on superceded or historical calculations and resulted
in many of the CRs on design basis calculational issues not being found.  


    Analysis: The team determined that a performance deficiency existed because the
Enclosure
    licensee failed to adequately assess and justify the downgrade of a condition adverse to
77
    quality as required by procedure NOP-LP-2001. Since there was a performance
Analysis: The team determined that a performance deficiency existed because the
    deficiency, the team compared this performance deficiency to the minor questions
licensee failed to adequately assess and justify the downgrade of a condition adverse to
    contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
quality as required by procedure NOP-LP-2001. Since there was a performance
    Reports." The team concluded that the performance deficiency was minor because the
deficiency, the team compared this performance deficiency to the minor questions
    team did not identify other examples where downgrades were performed without
contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection
    adequate justification and because no specific calculation deficiencies which resulted in
Reports." The team concluded that the performance deficiency was minor because the
    inoperable equipment were associated with the CR.
team did not identify other examples where downgrades were performed without
    Enforcement: The failure to provide adequate justification when downgrading a SCAQ
adequate justification and because no specific calculation deficiencies which resulted in
    constitutes a violation of 10 CFR Part 50, Appendix B, Criterion V. However, this
inoperable equipment were associated with the CR.  
    violation was determined to have minor significance and is not subject to enforcement
Enforcement: The failure to provide adequate justification when downgrading a SCAQ
    action in accordance with Section IV of the NRCs Enforcement Policy. The licensee
constitutes a violation of 10 CFR Part 50, Appendix B, Criterion V. However, this
    documented the issue in CR 03-06948.
violation was determined to have minor significance and is not subject to enforcement
    While minor violations are not normally documented in inspection reports, the team
action in accordance with Section IV of the NRCs Enforcement Policy. The licensee
    determined that documentation was appropriate in this case due the underlying cause is
documented the issue in CR 03-06948.
    similar to that of other findings in this report.
While minor violations are not normally documented in inspection reports, the team
.23 Inappropriate Application of 10 CFR 50.59
determined that documentation was appropriate in this case due the underlying cause is
    Introduction: The team identified a NCV of 10 CFR 50.59, Changes, Tests and
similar to that of other findings in this report.
    Experiments. Specifically, the licensee failed to preform an adequate evaluation of a
    .23 Inappropriate Application of 10 CFR 50.59
    defacto modification to the plant where the underlying change may have required NRC
Introduction: The team identified a NCV of 10 CFR 50.59, Changes, Tests and
    approval prior to implementation. Following discovery, the licensee entered the issue
Experiments. Specifically, the licensee failed to preform an adequate evaluation of a
    into its corrective action program and re-performed the evaluation; the licensee also
defacto modification to the plant where the underlying change may have required NRC
    repaired those barriers which were physically degraded. The primary cause of this
approval prior to implementation. Following discovery, the licensee entered the issue
    violation was related to the cross-cutting area of human performance as the licensee
into its corrective action program and re-performed the evaluation; the licensee also
    appeared to selectively choosing information from the guidance document.
repaired those barriers which were physically degraded. The primary cause of this
    Description: In IR 05000346/2002019, LER 05000346/2002-006 was closed and an URI
violation was related to the cross-cutting area of human performance as the licensee
    was opened to track resolution of safety related structures which were unprotected
appeared to selectively choosing information from the guidance document.
    against tornado missiles; specifically that six feet of the EDG exhaust stacks were
Description: In IR 05000346/2002019, LER 05000346/2002-006 was closed and an URI
    unprotected and that portions of a concrete barrier were degraded. This issue was
was opened to track resolution of safety related structures which were unprotected
    being tracked in the licensee's corrective action system under CRs 02-04146, 02-04147,
against tornado missiles; specifically that six feet of the EDG exhaust stacks were
    02-04700 and 02-05590. The team determined that the licensee had evaluated the
unprotected and that portions of a concrete barrier were degraded. This issue was
    non-conforming conditions using a computer code (TORMIS) discussed in Electric
being tracked in the licensee's corrective action system under CRs 02-04146, 02-04147,
    Power Research Institute (EPRI) Topical Report NP-2005, "Tornado Missile Risk
02-04700 and 02-05590. The team determined that the licensee had evaluated the
    Evaluation Methodology," Volumes I and II, August 1981. Based on use of this code,
non-conforming conditions using a computer code (TORMIS) discussed in Electric
    the licensee determined the probability of the unprotected areas being struck by a
Power Research Institute (EPRI) Topical Report NP-2005, "Tornado Missile Risk
    tornado missile was relatively low.
Evaluation Methodology," Volumes I and II, August 1981. Based on use of this code,
    The licensee revised the USAR to incorporate the TORMIS methodology, including a
the licensee determined the probability of the unprotected areas being struck by a
    provision which allowed it to be used to accept degraded or non-conforming conditions.
tornado missile was relatively low.
    On that basis, the licensee declared the diesel generators operable and determined that
The licensee revised the USAR to incorporate the TORMIS methodology, including a
    repairs were not needed for the non-conforming structures until 2004. In regard to the
provision which allowed it to be used to accept degraded or non-conforming conditions.  
    unprotected stacks, the licensee determined that no modifications were necessary.
On that basis, the licensee declared the diesel generators operable and determined that
                                                77                                  Enclosure
repairs were not needed for the non-conforming structures until 2004. In regard to the
unprotected stacks, the licensee determined that no modifications were necessary.


Enclosure
78
Prior to the USAR change, Section 3.5.1 of the USAR stated that, "Protection against a
Prior to the USAR change, Section 3.5.1 of the USAR stated that, "Protection against a
potential missile may be provided by, but not necessarily limited to, any one or
potential missile may be provided by, but not necessarily limited to, any one or
combination of the following protection methods: compartmentalization, barriers,
combination of the following protection methods: compartmentalization, barriers,
separation, distance, restraints, strategic orientation and equipment design." The team
separation, distance, restraints, strategic orientation and equipment design." The team
noted that all these methods involved physical protection of the equipment, rather than
noted that all these methods involved physical protection of the equipment, rather than
methods of evaluation. Under change notice 02-063, the licensee changed this
methods of evaluation. Under change notice 02-063, the licensee changed this
statement to add tornado missile probability as a protection method.
statement to add tornado missile probability as a protection method.
As part of the USAR change, the licensee performed an evaluation as required by
As part of the USAR change, the licensee performed an evaluation as required by
10 CFR 50.59. During review of this evaluation, the team questioned whether the
10 CFR 50.59. During review of this evaluation, the team questioned whether the
licensee had appropriately followed the guidance in Nuclear Energy Institute standard
licensee had appropriately followed the guidance in Nuclear Energy Institute standard
NEI 96-07, which NRC endorsed in Regulatory Guide 1.187. Specifically, the licensee
NEI 96-07, which NRC endorsed in Regulatory Guide 1.187. Specifically, the licensee
appeared to be incorporating use of the TORMIS methodology, using the methodology
appeared to be incorporating use of the TORMIS methodology, using the methodology
to accept a defacto change to the plant (where the plant did not match the description in
to accept a defacto change to the plant (where the plant did not match the description in
the USAR) and then justifying the methodologys use for future non-conforming or
the USAR) and then justifying the methodologys use for future non-conforming or
degraded conditions all in the same 50.59 evaluation. The team noted that these
degraded conditions all in the same 50.59 evaluation. The team noted that these
differing applications affected how the 10 CFR 50.59, Section c.2, questions were
differing applications affected how the 10 CFR 50.59, Section c.2, questions were
answered in the licensees 10 CFR 50.59 evaluation. The team also noted that the
answered in the licensees 10 CFR 50.59 evaluation. The team also noted that the
questions were answered based on the standard review plan, rather than on the
questions were answered based on the standard review plan, rather than on the
Davis-Besse USAR.
Davis-Besse USAR.
Line 3,953: Line 4,368:
the TORMIS methodology was an "approved methodology and, therefore, wasnt a
the TORMIS methodology was an "approved methodology and, therefore, wasnt a
departure from a method of evaluation described in the FSAR (as updated) used in
departure from a method of evaluation described in the FSAR (as updated) used in
establishing the design bases or in the safety analyses" as defined in 10 CFR 50.59.
establishing the design bases or in the safety analyses" as defined in 10 CFR 50.59.  
However, the team noted that there was not an existing method of evaluation that
However, the team noted that there was not an existing method of evaluation that
applied to protection of the EDGs. Instead, the change was from "protection by means
applied to protection of the EDGs. Instead, the change was from "protection by means
of a physical barrier," to "protection by means of a probabilistic approach," which
of a physical barrier," to "protection by means of a probabilistic approach," which
appeared to have introduced a new failure mode not previously evaluated for the EDGs.
appeared to have introduced a new failure mode not previously evaluated for the EDGs.  
The introduction of this new failure mode did not appear to be addressed by the
The introduction of this new failure mode did not appear to be addressed by the
licensees 50.59 evaluation.
licensees 50.59 evaluation.
Specifically, the USAR previously stated that the diesel generators were not affected by
Specifically, the USAR previously stated that the diesel generators were not affected by
tornado generated missiles due to physical features. Inclusion of the TORMIS
tornado generated missiles due to physical features. Inclusion of the TORMIS
methodology introduced the possibility that the diesels could be affected by tornado
methodology introduced the possibility that the diesels could be affected by tornado
generated missiles. The licensee answered this question in its 10 CFR 50.59 evaluation
generated missiles. The licensee answered this question in its 10 CFR 50.59 evaluation
by stating that "the probability of a tornado generated missile was incredible, that NRC
by stating that "the probability of a tornado generated missile was incredible, that NRC
accepted use of probability for Davis-Besse in analyzing the probability that turbine
accepted use of probability for Davis-Besse in analyzing the probability that turbine
Line 3,970: Line 4,385:
However, the team noted the following guidance in NEI 96-07, Section 4.3.6:
However, the team noted the following guidance in NEI 96-07, Section 4.3.6:
"Malfunctions of SSCs are generally postulated as potential single failures to evaluate
"Malfunctions of SSCs are generally postulated as potential single failures to evaluate
                                          78                                    Enclosure


Enclosure
79
plant performance with the focus being on the result of the malfunction rather than the
plant performance with the focus being on the result of the malfunction rather than the
cause or type of malfunction. A malfunction that involves an initiator or failure whose
cause or type of malfunction. A malfunction that involves an initiator or failure whose
effects are not bounded by those explicitly described in the USAR is a malfunction with a
effects are not bounded by those explicitly described in the USAR is a malfunction with a
different result..."
different result..."
Line 3,981: Line 4,397:
been answered "yes" and prior NRC review of this change sought.
been answered "yes" and prior NRC review of this change sought.
At the end of the inspection, the licensee had written a new CR, 03-06561, and was
At the end of the inspection, the licensee had written a new CR, 03-06561, and was
revising the 10 CFR 50.59 evaluation to address the above issues. The revised 10 CFR
revising the 10 CFR 50.59 evaluation to address the above issues. The revised 10 CFR
50.59 analysis was not reviewed by the team.
50.59 analysis was not reviewed by the team.
The team also noted that the licensee had to physically repair the degraded concrete to
The team also noted that the licensee had to physically repair the degraded concrete to
restore its tornado protection capability. The licensee had not considered these physical
restore its tornado protection capability. The licensee had not considered these physical
changes necessary until the team identified the concern regarding inappropriately using
changes necessary until the team identified the concern regarding inappropriately using
10 CFR 50.59 to correct non-conforming or degraded conditions. However, new
10 CFR 50.59 to correct non-conforming or degraded conditions. However, new
physical barriers for tornado missile protection were not added to those areas which
physical barriers for tornado missile protection were not added to those areas which
initially lacked such barriers.
initially lacked such barriers.
Analysis: This issue was determined to involve a performance deficiency because the
Analysis: This issue was determined to involve a performance deficiency because the
licensee misapplied the criteria of 10 CFR 50.59 and concluded that prior NRC approval
licensee misapplied the criteria of 10 CFR 50.59 and concluded that prior NRC approval
was not required when such a conclusion could not be supported by the documented
was not required when such a conclusion could not be supported by the documented
50.59 evaluation. Because violations of 10 CFR 50.59 are considered to be violations
50.59 evaluation. Because violations of 10 CFR 50.59 are considered to be violations
that potentially impede or impact the regulatory process, they are dispositioned using
that potentially impede or impact the regulatory process, they are dispositioned using
the traditional enforcement process instead of the SDP. Typically, the Severity Level
the traditional enforcement process instead of the SDP. Typically, the Severity Level
would be assigned after consideration of appropriate factors for the particular regulatory
would be assigned after consideration of appropriate factors for the particular regulatory
process violation in accordance with the NRC Enforcement Policy. However, the SDP is
process violation in accordance with the NRC Enforcement Policy. However, the SDP is
used, if applicable, in order to consider the associated risk significance of the finding
used, if applicable, in order to consider the associated risk significance of the finding
prior to assigning a severity level. Using IMC 0612, Appendix B, "Issue Screening," the
prior to assigning a severity level. Using IMC 0612, Appendix B, "Issue Screening," the
team determined that the finding was more than minor because physical barriers were
team determined that the finding was more than minor because physical barriers were
degraded or missing and because those barriers being degraded could result in one or
degraded or missing and because those barriers being degraded could result in one or
more of the diesel generators failing to fulfill their design function during a tornado. This
more of the diesel generators failing to fulfill their design function during a tornado. This
was a design issue which affected the mitigating systems cornerstone.
was a design issue which affected the mitigating systems cornerstone.
The team reviewed this finding in accordance with IMC 0609, "Significance Determination
The team reviewed this finding in accordance with IMC 0609, "Significance Determination
Process. The consequence of the design was assessed through Phase 1 of the SDP.
Process. The consequence of the design was assessed through Phase 1 of the SDP.  
The team answered the question, "Does this issue involve an actual loss of safety
The team answered the question, "Does this issue involve an actual loss of safety
function," as "Yes," because under a design basis tornado, the diesel generator exhaust
function," as "Yes," because under a design basis tornado, the diesel generator exhaust
stacks were not physically protected. Based on this premise, the team entered Phase 2
stacks were not physically protected. Based on this premise, the team entered Phase 2
of the SDP.
of the SDP.
The team determined that the only event tree affected was LOOP concurrent with loss
The team determined that the only event tree affected was LOOP concurrent with loss
of one EDG. This was based on the assumption that a tornado missile hitting both EDG
of one EDG. This was based on the assumption that a tornado missile hitting both EDG
exhaust stacks would be an incredible event. The team decreased the initiating event
exhaust stacks would be an incredible event. The team decreased the initiating event
frequency from a "5" (once in 100,000 years) to a "3" (once in 1,000 years) based on the
frequency from a "5" (once in 100,000 years) to a "3" (once in 1,000 years) based on the
fact that the Davis-Besse switchyard was struck by a tornado in 1998 (in this event,
fact that the Davis-Besse switchyard was struck by a tornado in 1998 (in this event,
EDG 1 did not start from the control room and was declared technically inoperable due
EDG 1 did not start from the control room and was declared technically inoperable due
                                          79                                        Enclosure


    to the room design basis temperature of 120EF being exceeded). In reviewing the 1998
Enclosure
    event, the team determined that one turbine driven AFW pump was out of service for
80
    maintenance. Therefore, the team assumed that a turbine driven AFW pump was out of
to the room design basis temperature of 120F being exceeded). In reviewing the 1998
    service for purposes for the Phase 2 analysis. Based on these credible assumptions,
event, the team determined that one turbine driven AFW pump was out of service for
    the technical issue was determined to have very low safety significance and the violation
maintenance. Therefore, the team assumed that a turbine driven AFW pump was out of
    is categorized as Severity Level IV.
service for purposes for the Phase 2 analysis. Based on these credible assumptions,
    Enforcement: Title 10 CFR 50.59(d)(1) requires that the licensees maintain records of
the technical issue was determined to have very low safety significance and the violation
    changes in the facility, of changes in procedures, and of tests and experiments made
is categorized as Severity Level IV.
    pursuant to 10 CFR 50.59(c). It further requires that these records include a written
Enforcement: Title 10 CFR 50.59(d)(1) requires that the licensees maintain records of
    evaluation which provides the bases for the determination that the change, test or
changes in the facility, of changes in procedures, and of tests and experiments made
    experiment does not require a license amendment pursuant to 10 CFR 50.59(c)(2).
pursuant to 10 CFR 50.59(c). It further requires that these records include a written
    Contrary to the above, on November 7, 2002, the licensee approved a 50.59 evaluation
evaluation which provides the bases for the determination that the change, test or
    incorporating a change in the design basis to accept not physically protecting the EDG
experiment does not require a license amendment pursuant to 10 CFR 50.59(c)(2).
    exhaust stacks from tornado missiles. However, the evaluation did not provide the basis
Contrary to the above, on November 7, 2002, the licensee approved a 50.59 evaluation
    for why a possibility for a malfunction of the diesel generators due to impact on the
incorporating a change in the design basis to accept not physically protecting the EDG
    diesel generator exhaust stacks by a tornado missile did not produce a different result
exhaust stacks from tornado missiles. However, the evaluation did not provide the basis
    than any previously evaluated in the final safety analysis report.
for why a possibility for a malfunction of the diesel generators due to impact on the
    The failure to provide a written evaluation which described the basis for concluding a
diesel generator exhaust stacks by a tornado missile did not produce a different result
    license amendment was not needed was a violation of 10 CFR 50.59(d)(1). This issue
than any previously evaluated in the final safety analysis report.  
    has been entered into the licensees CAP as CR 03-06561. This Severity Level IV
The failure to provide a written evaluation which described the basis for concluding a
    violation is being treated as an NCV consistent with Section VI.A.1 of the NRC
license amendment was not needed was a violation of 10 CFR 50.59(d)(1). This issue
    Enforcement Policy. (NCV 05000346/2003010-23)
has been entered into the licensees CAP as CR 03-06561. This Severity Level IV
.24 Failure to Perform Comprehensive Moderate Energy Line Break Analysis
violation is being treated as an NCV consistent with Section VI.A.1 of the NRC
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
Enforcement Policy. (NCV 05000346/2003010-23)
    having very low safety significance (Green). Specifically, the licensee failed to include
    .24 Failure to Perform Comprehensive Moderate Energy Line Break Analysis
    the environmental effects of a DHR pump seal failure in its moderate energy line break
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    analysis. Following discovery, the licensee entered the issue into its corrective action
having very low safety significance (Green). Specifically, the licensee failed to include
    program and performed the analysis.
the environmental effects of a DHR pump seal failure in its moderate energy line break
    Description: The licensee initiated CR 02-07757 to document the failure to perform a
analysis. Following discovery, the licensee entered the issue into its corrective action
    comprehensive moderate energy line break analysis. This CR was rolled over into
program and performed the analysis.
    CR 02-06370, which required that the concerns of additional heat generation caused by
Description: The licensee initiated CR 02-07757 to document the failure to perform a
    the moderate energy line break (DHR pump seal) be addressed in the new calculation
comprehensive moderate energy line break analysis. This CR was rolled over into
    being performed in response to CR 02-06370. The team determined that the heat load
CR 02-06370, which required that the concerns of additional heat generation caused by
    caused by failure of the DHR pump seal (an additional 21,000 btu/hr) was included in
the moderate energy line break (DHR pump seal) be addressed in the new calculation
    calculation C-NSA-032.02-006 and that the discrepant condition was adequately
being performed in response to CR 02-06370. The team determined that the heat load
    resolved.
caused by failure of the DHR pump seal (an additional 21,000 btu/hr) was included in
    Analysis: The team determined that a performance deficiency existed because the
calculation C-NSA-032.02-006 and that the discrepant condition was adequately
    licensee failed to have a design analysis to demonstrate the ability to withstand
resolved.
    moderate energy line breaks as specified in design documents. Since there was a
Analysis: The team determined that a performance deficiency existed because the
    performance deficiency, the team compared this performance deficiency to the minor
licensee failed to have a design analysis to demonstrate the ability to withstand
    questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
moderate energy line breaks as specified in design documents. Since there was a
    Inspection Reports." The team concluded that the issue was more than minor because
performance deficiency, the team compared this performance deficiency to the minor
                                              80                                    Enclosure
questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
Inspection Reports." The team concluded that the issue was more than minor because


    the licensee had to perform calculations to show that the environmental effects were
Enclosure
    acceptable. This was a design issue which affected the mitigating systems cornerstone.
81
    The team reviewed this finding in accordance with IMC 0609, "Significance
the licensee had to perform calculations to show that the environmental effects were
    Determination Process, and, based on the determination that the moderate energy line
acceptable. This was a design issue which affected the mitigating systems cornerstone.  
    break heat loads were acceptable and that the system could perform its design function,
The team reviewed this finding in accordance with IMC 0609, "Significance
    answered no to all five screening questions in the Phase 1 Screening Worksheet
Determination Process, and, based on the determination that the moderate energy line
    under the Mitigating Systems column. The team concluded the issue was of very low
break heat loads were acceptable and that the system could perform its design function,
    safety significance (Green).
answered no to all five screening questions in the Phase 1 Screening Worksheet
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
under the Mitigating Systems column. The team concluded the issue was of very low
    measures be established to assure that applicable regulatory requirements and the
safety significance (Green).
    design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
    instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
    checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
    use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
    testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
    Contrary to the above, the licensee failed to translate the consequences of leakage from
use of alternate or simplified calculational methods, or by the performance of a suitable
    the DHR pump seals into calculations of record for moderate energy line breaks. The
testing program.
    licensee entered the issue into its CAP as CRs 02-07757 and 02-06370. Because this
Contrary to the above, the licensee failed to translate the consequences of leakage from
    violation was of very low safety significance and because it was entered into the
the DHR pump seals into calculations of record for moderate energy line breaks. The
    licensees CAP, this violation is being treated as an NCV consistent with Section VI.A of
licensee entered the issue into its CAP as CRs 02-07757 and 02-06370. Because this
    the NRC Enforcement Policy. (NCV 05000346/2003010-24)
violation was of very low safety significance and because it was entered into the
(4) Detailed Team Review of Licensee Corrective Actions Implemented to Address
licensees CAP, this violation is being treated as an NCV consistent with Section VI.A of
    Operational Issues Previously Identified by the Licensee
the NRC Enforcement Policy. (NCV 05000346/2003010-24)
a. Inspection Scope
(4)
    The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,
Detailed Team Review of Licensee Corrective Actions Implemented to Address
    and resolve the identified equipment, human performance or programmatic adverse to
Operational Issues Previously Identified by the Licensee
    quality plant conditions. The team mainly focused on plant systems design and
  a.
    licensing basis requirements issues which were previously identified by the NRC, the
Inspection Scope
    licensee and others during various design reviews conducted in 2002. The team
The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,
    assessed effectiveness of the licensees corrective actions implemented to address
and resolve the identified equipment, human performance or programmatic adverse to
    previously identified operational issues.
quality plant conditions. The team mainly focused on plant systems design and
b. Findings
licensing basis requirements issues which were previously identified by the NRC, the
    Repetitive Spacer Grid Strap Damage
licensee and others during various design reviews conducted in 2002. The team
    Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
assessed effectiveness of the licensees corrective actions implemented to address
    having very low safety significance (Green). Specifically, the licensee failed to take
previously identified operational issues.
    adequate corrective actions to previous events to prevent damage to a new fuel
  b.
    assembly spacer grid strap during the final reload of the core in 2003. Following
Findings
    discovery, the licensee entered the issue into its corrective action program. The primary
Repetitive Spacer Grid Strap Damage
    cause of this violation was related to the cross-cutting areas of corrective action and
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,
    human performance, because, despite earlier events, the licensee failed to adequately
having very low safety significance (Green). Specifically, the licensee failed to take
                                              81                                      Enclosure
adequate corrective actions to previous events to prevent damage to a new fuel
assembly spacer grid strap during the final reload of the core in 2003. Following
discovery, the licensee entered the issue into its corrective action program. The primary
cause of this violation was related to the cross-cutting areas of corrective action and
human performance, because, despite earlier events, the licensee failed to adequately


Enclosure
82
address the human performance issues that contributed to this and other fuel spacer
address the human performance issues that contributed to this and other fuel spacer
grid events.
grid events.
Description: The licensee designated CR 02-06178 as a SCAQ CR. This CR described
Description: The licensee designated CR 02-06178 as a SCAQ CR. This CR described
repetitive damage to fuel assembly grid straps and rolled in the following CRs:
repetitive damage to fuel assembly grid straps and rolled in the following CRs:
02-05645, 02-05895, 02-05896, 02-06343, and 02-09829. A root cause report was
02-05645, 02-05895, 02-05896, 02-06343, and 02-09829. A root cause report was
required for CR 02-06178 as part of a NQA stop work order on fuel movements.
required for CR 02-06178 as part of a NQA stop work order on fuel movements.
REVIEW OF ROOT CAUSE REPORT: The licensee issued a root cause analysis in
REVIEW OF ROOT CAUSE REPORT: The licensee issued a root cause analysis in
January 2003 which determined the cause of the repetitive grid strap damage. At this
January 2003 which determined the cause of the repetitive grid strap damage. At this
time, the licensees CAP did not require use of a formal root cause process; however, a
time, the licensees CAP did not require use of a formal root cause process; however, a
formal TAPROOT process was used. Also, in May 2002, the licensee had completed a
formal TAPROOT process was used. Also, in May 2002, the licensee had completed a
root cause of fuel damage identified earlier in the outage. In reviewing the
root cause of fuel damage identified earlier in the outage. In reviewing the
January 2003 root cause report, the team noted several deficiencies:
January 2003 root cause report, the team noted several deficiencies:
*       The discussion on what occurred appeared to rely extensively on the previous
*
        root cause, performed in May 2002, and on a 1999 Babcock and Wilcox (B&W)
The discussion on what occurred appeared to rely extensively on the previous
        root cause. The explanations for the statements made in the January 2003
root cause, performed in May 2002, and on a 1999 Babcock and Wilcox (B&W)
        report required understanding of the earlier studies in order to comprehend their
root cause. The explanations for the statements made in the January 2003
        applicability.
report required understanding of the earlier studies in order to comprehend their
*       The January 2003 root cause primarily focused on the new fuel assembly which
applicability.
        was discovered to be damaged in September 2002. It limited its discussion of
*
        the other fuel assemblies discovered to be damaged in the September 2002 time
The January 2003 root cause primarily focused on the new fuel assembly which
        frame to listing the damage in a table and describing the disposition. This was
was discovered to be damaged in September 2002. It limited its discussion of
        despite these CRs for these fuel assemblies being "rolled into" the root cause
the other fuel assemblies discovered to be damaged in the September 2002 time
        report and a corrective action entry being closed with a statement that the root
frame to listing the damage in a table and describing the disposition. This was
        cause report addressed the damage to the fuel assemblies.
despite these CRs for these fuel assemblies being "rolled into" the root cause
*       The team noted that ten fuel assemblies were discovered to be damaged in
report and a corrective action entry being closed with a statement that the root
        September through December 2002. This was in addition to the seven fuel
cause report addressed the damage to the fuel assemblies.
        assemblies discovered to be damaged in March 2002. In one place in the
*
        January 2003 root cause report, the licensee stated that the damage had to
The team noted that ten fuel assemblies were discovered to be damaged in
        occur during RFO 12, because there was no oxidation on fuel assemblies. The
September through December 2002. This was in addition to the seven fuel
        team ascertained that, if the first statement was true, then the extent of condition
assemblies discovered to be damaged in March 2002. In one place in the
        for the May 2002 root cause report must have been deficient in that it failed to
January 2003 root cause report, the licensee stated that the damage had to
        identify a number of damaged fuel assemblies.
occur during RFO 12, because there was no oxidation on fuel assemblies. The
*       In another section, the root cause report stated that review of the core loading
team ascertained that, if the first statement was true, then the extent of condition
        sequence determined that assembly NJ125Y, "and a number of other
for the May 2002 root cause report must have been deficient in that it failed to
        assemblies," were loaded in a sequence that exposed those assemblies to
identify a number of damaged fuel assemblies.
        undesired corner to corner interactions. This second statement implied that the
*
        damage might well have occurred during the fuel shuffle in March 2002.
In another section, the root cause report stated that review of the core loading
        However, the root cause report did not specifically identify which assemblies
sequence determined that assembly NJ125Y, "and a number of other
        were so loaded or otherwise follow up on this comment. The team determined
assemblies," were loaded in a sequence that exposed those assemblies to
        that a possible contributing cause was not identified or corrected.
undesired corner to corner interactions. This second statement implied that the
*       The team noted that eight of the ten fuel assemblies discovered to be damaged
damage might well have occurred during the fuel shuffle in March 2002.  
        in September through December had only been burned once, and two were new
However, the root cause report did not specifically identify which assemblies
                                          82                                      Enclosure
were so loaded or otherwise follow up on this comment. The team determined
that a possible contributing cause was not identified or corrected.
*
The team noted that eight of the ten fuel assemblies discovered to be damaged
in September through December had only been burned once, and two were new


          fuel assemblies. Thus, the assemblies should not have been overly "bowed and
Enclosure
          twisted," although this was listed as a possible reason for the damage.
83
  *       In regard to the extent of condition, the team noted that the licensee provided an
fuel assemblies. Thus, the assemblies should not have been overly "bowed and
          extensive list of damage which occurred at other B&W sites. However, the only
twisted," although this was listed as a possible reason for the damage.
          Davis-Besse information from previous outages was from cycle 11. Data from
*
          cycle 12 was missing from the table.
In regard to the extent of condition, the team noted that the licensee provided an
  *       Based on the information in the extent of condition table, the team noted that,
extensive list of damage which occurred at other B&W sites. However, the only
          approximately the same number of fuel assemblies were involved in both RFO
Davis-Besse information from previous outages was from cycle 11. Data from
          11 and 13. However, in RFO 11 the damaged fuel was mostly burned multiple
cycle 12 was missing from the table.
          times and to have damage to only one or two grid strap locations. In RFO 13
*
          (the current outage), the damaged fuel was primarily unburned or burned only
Based on the information in the extent of condition table, the team noted that,
          once and had damage to multiple grid strap locations.
approximately the same number of fuel assemblies were involved in both RFO
  *       The discussion on the December grid strap damage gave little credence to the
11 and 13. However, in RFO 11 the damaged fuel was mostly burned multiple
          report that the fuel assembly was undamaged in September. Instead a
times and to have damage to only one or two grid strap locations. In RFO 13
          statement was made that because spacer grid 2 was damaged, and it hadn't
(the current outage), the damaged fuel was primarily unburned or burned only
          entered the pool, the damage must have occurred earlier. Given the extent of
once and had damage to multiple grid strap locations.
          the damage to the fuel assembly, the information provided in the CR initiation
*
          statement from the personnel present, and the fact that only the northeast corner
The discussion on the December grid strap damage gave little credence to the
          face was damaged, the team considered it more likely that the damage occurred
report that the fuel assembly was undamaged in September. Instead a
          all at one time.
statement was made that because spacer grid 2 was damaged, and it hadn't
*         The root cause report did not provide any discussion of the impact that occurred
entered the pool, the damage must have occurred earlier. Given the extent of
          during the December re-insertion. The team considered it unlikely that the
the damage to the fuel assembly, the information provided in the CR initiation
          impact would not have caused any damage. The team noted that CR 02-09829
statement from the personnel present, and the fact that only the northeast corner
          stated that the assembly visibly moved to the south. The team also noted that all
face was damaged, the team considered it more likely that the damage occurred
          the damage occurred on the northeast corner. This indicated to the team that
all at one time.
          the damage likely occurred during the re-insertion since a deflection to the south
*
          would be an expected result if the northeast corner of the fuel assembly
The root cause report did not provide any discussion of the impact that occurred
          impacted the cell. The failure to address why the impact occurred and the result
during the December re-insertion. The team considered it unlikely that the
          of the impact appeared to be a significant weakness in the root cause.
impact would not have caused any damage. The team noted that CR 02-09829
  *       The team determined that no mention was made in the root cause report of
stated that the assembly visibly moved to the south. The team also noted that all
          items such as whether the fuel handling personnel had the mast in fast or slow
the damage occurred on the northeast corner. This indicated to the team that
          speed or what the routine practice was regarding the fuel insertion rate.
the damage likely occurred during the re-insertion since a deflection to the south
          Additionally, items such as length of time the crew had been working, schedule
would be an expected result if the northeast corner of the fuel assembly
          pressures, and other factors which would address human performance were not
impacted the cell. The failure to address why the impact occurred and the result
          discussed, although these all could play a role in fuel handling mishaps.
of the impact appeared to be a significant weakness in the root cause.
  FEBRUARY DAMAGE TO NEW FUEL ASSEMBLY: On February 24, 2003, during the final
*
  reload of the cycle 14 core, another new fuel assembly was damaged. This was
The team determined that no mention was made in the root cause report of
  documented in CR 03-01492. The licensee did an apparent cause evaluation for this
items such as whether the fuel handling personnel had the mast in fast or slow
  event and concluded that the damage to this fuel assembly was likely due to the less
speed or what the routine practice was regarding the fuel insertion rate.  
  than adequate design of the fuel assemblies. The team noted a number of issues that
Additionally, items such as length of time the crew had been working, schedule
  did not appear to have been adequately considered in reaching the apparent cause
pressures, and other factors which would address human performance were not
  conclusion. For example:
discussed, although these all could play a role in fuel handling mishaps.
                                            83                                    Enclosure
FEBRUARY DAMAGE TO NEW FUEL ASSEMBLY: On February 24, 2003, during the final
reload of the cycle 14 core, another new fuel assembly was damaged. This was
documented in CR 03-01492. The licensee did an apparent cause evaluation for this
event and concluded that the damage to this fuel assembly was likely due to the less
than adequate design of the fuel assemblies. The team noted a number of issues that
did not appear to have been adequately considered in reaching the apparent cause
conclusion. For example:


*       The damage occurred after the majority of the fuel assemblies were loaded and
Enclosure
        only a few remained; this was not addressed in the apparent cause analysis.
84
*       The fuel handlers had spent approximately two hours unsuccessfully trying to
*
        load another fuel assembly into place before deciding to change the loading
The damage occurred after the majority of the fuel assemblies were loaded and
        sequence to load another assembly in a potential corner to corner interaction
only a few remained; this was not addressed in the apparent cause analysis.
        pattern. There was no indication that anyone suggested stopping the process
*
        and evaluating the condition, before agreeing to the change in the loading
The fuel handlers had spent approximately two hours unsuccessfully trying to
        sequence.
load another fuel assembly into place before deciding to change the loading
*       Over the next three hours, multiple problems were experienced as the licensee
sequence to load another assembly in a potential corner to corner interaction
        attempted to load the fuel assembly, including multiple overload conditions and
pattern. There was no indication that anyone suggested stopping the process
        cable oscillations. The licensee reset the overload setpoints to the least limiting
and evaluating the condition, before agreeing to the change in the loading
        condition at least twice, and even this setpoint was reached. Again, when
sequence.
        problems were encountered, the decision was to keep on trying to insert the
*
        assembly, rather than stopping and evaluating what was happening.
Over the next three hours, multiple problems were experienced as the licensee
Analysis: The team determined that a performance deficiency existed because the
attempted to load the fuel assembly, including multiple overload conditions and
cable oscillations. The licensee reset the overload setpoints to the least limiting
condition at least twice, and even this setpoint was reached. Again, when
problems were encountered, the decision was to keep on trying to insert the
assembly, rather than stopping and evaluating what was happening.
Analysis: The team determined that a performance deficiency existed because the
licensee failed to take adequate corrective actions in response to previous events and
licensee failed to take adequate corrective actions in response to previous events and
as a result, a new fuel assembly spacer grid strap was damaged during the final reload
as a result, a new fuel assembly spacer grid strap was damaged during the final reload
of the core in February 2003. Since there was a performance deficiency, the team
of the core in February 2003. Since there was a performance deficiency, the team
compared this performance deficiency to the minor questions contained in Appendix B,
compared this performance deficiency to the minor questions contained in Appendix B,
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team
concluded that the issue was more than minor because the licensee failed to prevent
concluded that the issue was more than minor because the licensee failed to prevent
recurrence of a significant condition adverse to quality as evidenced by damage to
recurrence of a significant condition adverse to quality as evidenced by damage to
previously undamaged fuel assembly grid straps. The team reviewed this finding in
previously undamaged fuel assembly grid straps. The team reviewed this finding in
accordance with IMC 0609, "Significance Determination Process. The barrier integrity
accordance with IMC 0609, "Significance Determination Process. The barrier integrity
cornerstone was affected as failure of the grid straps has led to fuel leaks. No other
cornerstone was affected as failure of the grid straps has led to fuel leaks. No other
cornerstones were affected. There was one SDP Phase 1 worksheet question relating
cornerstones were affected. There was one SDP Phase 1 worksheet question relating
to the fuel barrier. As this issue related to fuel barrier, the team concluded the issue
to the fuel barrier. As this issue related to fuel barrier, the team concluded the issue
was of very low safety significance (Green).
was of very low safety significance (Green).  
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
measures be established to ensure that conditions adverse to quality, such as
measures be established to ensure that conditions adverse to quality, such as
non-conformances, are promptly identified and corrected. For significant conditions
non-conformances, are promptly identified and corrected. For significant conditions
adverse to quality, it further requires that the cause is determined and corrective action
adverse to quality, it further requires that the cause is determined and corrective action
is taken to prevent recurrence.
is taken to prevent recurrence.
Contrary to the above, as of February 5, 2003, the licensee had failed to take corrective
Contrary to the above, as of February 5, 2003, the licensee had failed to take corrective
actions which prevented recurrence of grid strap damage, a significant condition
actions which prevented recurrence of grid strap damage, a significant condition
adverse to quality. Specifically on September 20, 2002, the licensee issued a stop work
adverse to quality. Specifically on September 20, 2002, the licensee issued a stop work
order and a SCAQ was identified and documented in CR 02-06178. The root cause for
order and a SCAQ was identified and documented in CR 02-06178. The root cause for
this report was completed in January 2003, prior to core reloading being allowed to
this report was completed in January 2003, prior to core reloading being allowed to
recommence. On February 5, a new fuel assembly was damaged after the licensee
recommence. On February 5, a new fuel assembly was damaged after the licensee
made multiple unsuccessful attempts to insert the assembly into the core.
made multiple unsuccessful attempts to insert the assembly into the core.
This issue was entered into the licensees CAP as CR 03-06996 at the end of the
This issue was entered into the licensees CAP as CR 03-06996 at the end of the
inspection. Because this violation was of very low safety significance and because it
inspection. Because this violation was of very low safety significance and because it
                                          84                                      Enclosure


      was entered into the licensees CAP, this violation is being treated as a NCV consistent
Enclosure
      with Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-25).
85
(5)   Review of Fire Protection Corrective Action Items
was entered into the licensees CAP, this violation is being treated as a NCV consistent
a.   Inspection Scope
with Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-25).
      The team reviewed the licensees CAP to identify and address 10 CFR Part 50,
(5)
      Appendix R, related deficiencies.
Review of Fire Protection Corrective Action Items
b.   Findings
  a.
  .1 Process Monitoring Function for Alternative Shutdown Capability
Inspection Scope
      Introduction: The team identified a Non-Cited violation of 10 CFR 50, Appendix R,
The team reviewed the licensees CAP to identify and address 10 CFR Part 50,
      Section III.L.2.d having very low safety significance. Specifically, the issue regarded the
Appendix R, related deficiencies.
      failure to provide necessary process monitoring readings for safe shutdown of the plant
  b.
      during a fire event. The primary cause of this violation was related to the cross-cutting
Findings
      area of problem identification and resolution because the licensee had previously
    .1
      identified this issue as an enhancement and did not recognize that it was a violation of
Process Monitoring Function for Alternative Shutdown Capability
      regulatory requirements.
Introduction: The team identified a Non-Cited violation of 10 CFR 50, Appendix R,
      Description: During a review of the fire protection program, the licensee issued
Section III.L.2.d having very low safety significance. Specifically, the issue regarded the
      CR 03-01648 identifying at failure to provide necessary process monitoring readings for
failure to provide necessary process monitoring readings for safe shutdown of the plant
      steam generator (SG) level and pressure necessary for safe shutdown of the plant
during a fire event. The primary cause of this violation was related to the cross-cutting
      during a fire event. For the limiting Appendix R scenario (control room or cable
area of problem identification and resolution because the licensee had previously
      spreading room fire) where alternative shutdown was required, SG instrumentation
identified this issue as an enhancement and did not recognize that it was a violation of
      would not have been available for the idle SG during safe shutdown of the plant.
regulatory requirements.
      Without this SG level and pressure instrumentation, licensee operators would not have
Description: During a review of the fire protection program, the licensee issued  
      been able to support the shell-tube differential temperature determination which was
CR 03-01648 identifying at failure to provide necessary process monitoring readings for
      required by the alternative shutdown procedure. This could have potentially resulted in
steam generator (SG) level and pressure necessary for safe shutdown of the plant
      the loss of the thermal communication between the tubes and shell of the idle SG
during a fire event. For the limiting Appendix R scenario (control room or cable
      resulting in unacceptable stresses on the tubes.
spreading room fire) where alternative shutdown was required, SG instrumentation
      Even though the alternative shutdown procedures did not contain the necessary
would not have been available for the idle SG during safe shutdown of the plant.  
      procedural steps to prevent this condition if a fire in these areas were to occur,
Without this SG level and pressure instrumentation, licensee operators would not have
      operators could have taken temperature readings using a volt-meter to record the
been able to support the shell-tube differential temperature determination which was
      temperatures locally at the penetration room. While these actions could not be credited
required by the alternative shutdown procedure. This could have potentially resulted in
      for the Appendix R analysis, they would be available. Additionally, after this
the loss of the thermal communication between the tubes and shell of the idle SG
      non-conformance was identified, the licensee performed a modification (ECR
resulting in unacceptable stresses on the tubes.
      03-0267-00) to provide level and pressure indication for the idle SG on the auxiliary
Even though the alternative shutdown procedures did not contain the necessary
      shutdown panel to support Appendix R safe shutdown.
procedural steps to prevent this condition if a fire in these areas were to occur,
      Analysis: The team determined that a performance deficiency existed because the
operators could have taken temperature readings using a volt-meter to record the
      licensee failed to provide SG level and pressure indication required for alternative
temperatures locally at the penetration room. While these actions could not be credited
      shutdown. Since there was a performance deficiency, the team compared this
for the Appendix R analysis, they would be available. Additionally, after this
      performance deficiency to the minor questions contained in Appendix B, "Issue
non-conformance was identified, the licensee performed a modification (ECR
      Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
03-0267-00) to provide level and pressure indication for the idle SG on the auxiliary
      that the issue was more than minor because it affected the initiating events cornerstone
shutdown panel to support Appendix R safe shutdown.
                                              85                                        Enclosure
Analysis: The team determined that a performance deficiency existed because the
licensee failed to provide SG level and pressure indication required for alternative
shutdown. Since there was a performance deficiency, the team compared this
performance deficiency to the minor questions contained in Appendix B, "Issue
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
that the issue was more than minor because it affected the initiating events cornerstone


  and, by not providing the direct indications necessary for the operators to determine the
Enclosure
  status of the idle SG, the probability of experiencing unacceptable stresses on the SG
86
  tubes during the limiting Appendix R scenario was increased.
and, by not providing the direct indications necessary for the operators to determine the
  The team reviewed this finding in accordance with IMC 0609, "Significance
status of the idle SG, the probability of experiencing unacceptable stresses on the SG
  Determination Process. The team determined this finding to be of very low
tubes during the limiting Appendix R scenario was increased.
  significance, based upon the low probability of a serious control room fire combined with
The team reviewed this finding in accordance with IMC 0609, "Significance
  the low probability that such a fire would affect this specific instrumentation
Determination Process. The team determined this finding to be of very low
  detrimentally. Additionally, even in the event that such a fire had affected this
significance, based upon the low probability of a serious control room fire combined with
  instrumentation, it was likely that the operators still would have been able to prevent
the low probability that such a fire would affect this specific instrumentation
  these tube stresses through use of manual actions, although this was not a credited
detrimentally. Additionally, even in the event that such a fire had affected this
  action in the Fire Protection procedures for this scenario. The team concluded the issue
instrumentation, it was likely that the operators still would have been able to prevent
  was of very low safety significance (Green).
these tube stresses through use of manual actions, although this was not a credited
  Enforcement: Title 10 CFR Part 50, Appendix R, Section III.L.2.d states, in part, that the
action in the Fire Protection procedures for this scenario. The team concluded the issue
  process monitoring function for the alternative shutdown capability shall be capable of
was of very low safety significance (Green).
  providing direct readings of the process variables necessary to perform and control the
Enforcement: Title 10 CFR Part 50, Appendix R, Section III.L.2.d states, in part, that the
  alternative shutdown.
process monitoring function for the alternative shutdown capability shall be capable of
  Contrary to the above, the licensee did not provide SG level and pressure indication that
providing direct readings of the process variables necessary to perform and control the
  was required for the alternative shutdown scenario for the control room or cable
alternative shutdown.
  spreading room fire. The licensee entered the issue into its CAP as CR 03-01648.
Contrary to the above, the licensee did not provide SG level and pressure indication that
  Because this violation was of very low safety significance and because it was entered
was required for the alternative shutdown scenario for the control room or cable
  into the licensees CAP, the violation is being treated as a NCV, consistent with
spreading room fire. The licensee entered the issue into its CAP as CR 03-01648.  
  Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-26)
Because this violation was of very low safety significance and because it was entered
.2 Supporting Functions for Alternative Shutdown Capability
into the licensees CAP, the violation is being treated as a NCV, consistent with  
  Introduction: The team identified a Non-Cited violation of 10 CFR Part 50, Appendix R,
Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-26)
  Section III.L.2.e having very low safety significance. Specifically, the licensee failed to
    .2
  provide the process cooling and lubrication necessary to permit the operation of the
Supporting Functions for Alternative Shutdown Capability
  equipment used for safe shutdown functions. The licensee entered the issue into its
Introduction: The team identified a Non-Cited violation of 10 CFR Part 50, Appendix R,
  corrective action program and performed a modification to resolve the issue. The
Section III.L.2.e having very low safety significance. Specifically, the licensee failed to
  primary cause of this violation was related to the cross-cutting area of problem
provide the process cooling and lubrication necessary to permit the operation of the
  identification and resolution because the licensee had previously identified this issue as
equipment used for safe shutdown functions. The licensee entered the issue into its
  an enhancement and did not recognize that it was a violation of regulatory requirements.
corrective action program and performed a modification to resolve the issue. The
  Description: During a control room fire scenario, the governing procedure,
primary cause of this violation was related to the cross-cutting area of problem
  DB-OP-02519, Serious Control Room Fire, could not have been performed as written.
identification and resolution because the licensee had previously identified this issue as
  During this scenario, the procedure directed the operator to restore containment cooling
an enhancement and did not recognize that it was a violation of regulatory requirements.
  by resetting the #1 and #3 CACs. However, because of a modification to the control
Description: During a control room fire scenario, the governing procedure,
  circuitry of these CACs, the reset button on the outside of the CAC switchgear cabinet
DB-OP-02519, Serious Control Room Fire, could not have been performed as written.  
  was rendered non-functional.
During this scenario, the procedure directed the operator to restore containment cooling
  Since the CACs were needed to ensure an acceptable containment atmosphere, without
by resetting the #1 and #3 CACs. However, because of a modification to the control
  them the potential existed that Appendix R credited equipment might not be functional
circuitry of these CACs, the reset button on the outside of the CAC switchgear cabinet
  during a control room fire scenario due to heightened temperatures in the containment.
was rendered non-functional.
  However, since the heatup in the containment was not instantaneous and since the
Since the CACs were needed to ensure an acceptable containment atmosphere, without
  equipment would have to be subject to the heightened temperatures for a relatively long
them the potential existed that Appendix R credited equipment might not be functional
                                            86                                      Enclosure
during a control room fire scenario due to heightened temperatures in the containment.  
However, since the heatup in the containment was not instantaneous and since the
equipment would have to be subject to the heightened temperatures for a relatively long


  period of time, the team considered it unlikely that the plant would have progressed to
Enclosure
  an unrecoverable condition prior to the operators being able to recover containment
87
  cooling. The licensee implemented a modification (ECR 03-0243-00) that rewired the
period of time, the team considered it unlikely that the plant would have progressed to
  control circuitry for CAC fan 1-1 such that, in the case of a control room fire, this fan
an unrecoverable condition prior to the operators being able to recover containment
  could be started in slow speed to provide cooling to the containment.
cooling. The licensee implemented a modification (ECR 03-0243-00) that rewired the
  Analysis: The team determined that a performance deficiency existed because the
control circuitry for CAC fan 1-1 such that, in the case of a control room fire, this fan
  licensee failed to provide containment air cooling for alternative shutdown. Since there
could be started in slow speed to provide cooling to the containment.
  was a performance deficiency, the team compared this performance deficiency to the
Analysis: The team determined that a performance deficiency existed because the
  minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
licensee failed to provide containment air cooling for alternative shutdown. Since there
  Reactor Inspection Reports." The team concluded that the issue was more than minor
was a performance deficiency, the team compared this performance deficiency to the
  because, if left uncorrected, the finding would become a more significant safety
minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power
  concern. By not providing containment air cooling as per the governing alternative
Reactor Inspection Reports." The team concluded that the issue was more than minor
  shutdown procedure, the probability of the failure of equipment relied upon for safe
because, if left uncorrected, the finding would become a more significant safety
  shutdown was increased. The team reviewed this finding in accordance with IMC 0609,
concern. By not providing containment air cooling as per the governing alternative
  "Significance Determination Process. The team assessed the finding through Phase 1
shutdown procedure, the probability of the failure of equipment relied upon for safe
  of the reactor safety mitigating systems SDP. This issue was screened to be of very low
shutdown was increased. The team reviewed this finding in accordance with IMC 0609,
  safety significance (Green) because there was not a total loss of safety function for an
"Significance Determination Process. The team assessed the finding through Phase 1
  assumed control room fire with evacuation. This was evaluated using the transient
of the reactor safety mitigating systems SDP. This issue was screened to be of very low
  without the secondary steam plant (TPCS) Phase 2 worksheet. Within the Phase 2
safety significance (Green) because there was not a total loss of safety function for an
  TPCS worksheet, the CAC supports the feed and bleed operation of the power operated
assumed control room fire with evacuation. This was evaluated using the transient
  relief valve (PORV) for decay heat removal if the SGs are not available. Given this fire
without the secondary steam plant (TPCS) Phase 2 worksheet. Within the Phase 2
  scenario, the PORV block valve would be closed by procedure and the PORV not used,
TPCS worksheet, the CAC supports the feed and bleed operation of the power operated
  so there was no effect on a safety function.
relief valve (PORV) for decay heat removal if the SGs are not available. Given this fire
  Enforcement: Title 10 CFR Part 50, Appendix R, Section III.L.2.e, states, in part, that
scenario, the PORV block valve would be closed by procedure and the PORV not used,
  supporting functions shall be capable of providing the process cooling, lubrication, etc.,
so there was no effect on a safety function.
  necessary to permit the operation of the equipment used for alternative safe shutdown
Enforcement: Title 10 CFR Part 50, Appendix R, Section III.L.2.e, states, in part, that
  functions.
supporting functions shall be capable of providing the process cooling, lubrication, etc.,
  Contrary to the above, the licensee did not adequately provide containment air cooling,
necessary to permit the operation of the equipment used for alternative safe shutdown
  because the governing procedure did not reflect a recent modification that disabled the
functions.
  Appendix R reset buttons for the #1 and #3 CACs. The CACs were required to support
Contrary to the above, the licensee did not adequately provide containment air cooling,
  operation of Appendix R equipment credited equipment. The licensee entered the issue
because the governing procedure did not reflect a recent modification that disabled the
  into its CAP as CR 03-02699 and 03-04341. Because this violation was of very low
Appendix R reset buttons for the #1 and #3 CACs. The CACs were required to support
  safety significance and because it was entered into the licensees CAP, the violation is
operation of Appendix R equipment credited equipment. The licensee entered the issue
  being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy.
into its CAP as CR 03-02699 and 03-04341. Because this violation was of very low
  (NCV 05000346/2003010-27)
safety significance and because it was entered into the licensees CAP, the violation is
.3 Emergency Diesel Generator Floor Drains Design Deficiency
being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy.  
  Introduction: The team identified a NCV of 10 CFR Part 50.48(a)(1), having very low
(NCV 05000346/2003010-27)
  safety significance (Green). Specifically, the licensee failed to evaluate the adequacy of
    .3
  EDG common floor drains following sprinkler system actuation in the fire affected EDG
Emergency Diesel Generator Floor Drains Design Deficiency
  room. Following discovery, the licensee entered the issue into its corrective action
Introduction: The team identified a NCV of 10 CFR Part 50.48(a)(1), having very low
  process and revised the fire response procedures to address the issue.
safety significance (Green). Specifically, the licensee failed to evaluate the adequacy of
  Description: The team determined that the floor drains between the two EDG rooms
EDG common floor drains following sprinkler system actuation in the fire affected EDG
  were common, and that they had insufficient drainage capacity. Preliminary calculations
room. Following discovery, the licensee entered the issue into its corrective action
                                            87                                      Enclosure
process and revised the fire response procedures to address the issue.
Description: The team determined that the floor drains between the two EDG rooms
were common, and that they had insufficient drainage capacity. Preliminary calculations


    by the licensee showed that the drains had a maximum capacity of 100 gpm, whereas
Enclosure
    the sprinkler system actuation resulted in 303 gpm in Room 318, and 286 gpm in
88
    Room 319.
by the licensee showed that the drains had a maximum capacity of 100 gpm, whereas
    Terminal blocks in both EDG control cabinets were located approximately seven inches
the sprinkler system actuation resulted in 303 gpm in Room 318, and 286 gpm in
    above floor level. The common drain lines between the EDG rooms would have allowed
Room 319.
    suppression system water from a fire in one EDG room to enter and affect the integrity
Terminal blocks in both EDG control cabinets were located approximately seven inches
    of the redundant EDG room. As a consequence of a fire in one EDG room with
above floor level. The common drain lines between the EDG rooms would have allowed
    sprinkler system actuation, water would have backed up in both EDG rooms and would
suppression system water from a fire in one EDG room to enter and affect the integrity
    have increased above the elevation of the terminal blocks within approximately 30
of the redundant EDG room. As a consequence of a fire in one EDG room with
    minutes. Furthermore, no operator or fire brigade instructions were in place to facilitate
sprinkler system actuation, water would have backed up in both EDG rooms and would
    drainage by opening of the doors to prevent equipment submergence. The licensee
have increased above the elevation of the terminal blocks within approximately 30
    initiated CRs 03-02577, 03-06901, and 03-07256 to document, evaluate, and disposition
minutes. Furthermore, no operator or fire brigade instructions were in place to facilitate
    these deficiencies in their CAP. As part of the corrective action, the licensee revised
drainage by opening of the doors to prevent equipment submergence. The licensee
    pre-fire plans AB-318 and AB-319 to provide compensatory measures to prevent
initiated CRs 03-02577, 03-06901, and 03-07256 to document, evaluate, and disposition
    flooding of the EDG rooms.
these deficiencies in their CAP. As part of the corrective action, the licensee revised
    Analysis: The team determined that a performance deficiency existed because the
pre-fire plans AB-318 and AB-319 to provide compensatory measures to prevent
    licensee failed to evaluate the adequacy of EDG common floor drains following sprinkler
flooding of the EDG rooms.
    system actuation. Since there was a performance deficiency, the team compared this
Analysis: The team determined that a performance deficiency existed because the
    performance deficiency to the minor questions contained in Appendix B, "Issue
licensee failed to evaluate the adequacy of EDG common floor drains following sprinkler
    Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
system actuation. Since there was a performance deficiency, the team compared this
    that the issue was more than minor because the finding affected the mitigating system
performance deficiency to the minor questions contained in Appendix B, "Issue
    cornerstone. This was a design deficiency that was confirmed not to result in the loss of
Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded
    function per Generic Letter 91-18, Revision 1. The team reviewed this finding in
that the issue was more than minor because the finding affected the mitigating system
    accordance with IMC 0609, "Significance Determination Process, and determined that
cornerstone. This was a design deficiency that was confirmed not to result in the loss of
    the issue was of very low safety significance (Green).
function per Generic Letter 91-18, Revision 1. The team reviewed this finding in
    Enforcement: Title 10 CFR 50.48(a)(1) requires, in part, that each operating nuclear
accordance with IMC 0609, "Significance Determination Process, and determined that
    power plant have a fire protection plan that satisfies Criterion III of 10 CFR Part 50,
the issue was of very low safety significance (Green).
    Appendix A. Criterion III, requires, in part, that fire-fighting systems shall be designed to
Enforcement: Title 10 CFR 50.48(a)(1) requires, in part, that each operating nuclear
    assure that their rupture or inadvertent operation does not significantly impair the safety
power plant have a fire protection plan that satisfies Criterion III of 10 CFR Part 50,
    capability of these structures, systems, and components.
Appendix A. Criterion III, requires, in part, that fire-fighting systems shall be designed to
    Contrary to the above, because the EDG common floor drains were not evaluated by the
assure that their rupture or inadvertent operation does not significantly impair the safety
    licensee, nor verified for adequacy following sprinkler system actuation, the potential
capability of these structures, systems, and components.
    existed for an inadvertent sprinkler system actuation or rupture to adversely affect the
Contrary to the above, because the EDG common floor drains were not evaluated by the
    capability of the EDGs to perform their safety function. The licensee entered this issue
licensee, nor verified for adequacy following sprinkler system actuation, the potential
    into its CAP as CRs 03-02577, 03-06901, and 03-07256. Because this violation was of
existed for an inadvertent sprinkler system actuation or rupture to adversely affect the
    very low safety significance and because it was entered into the licensees CAP, the
capability of the EDGs to perform their safety function. The licensee entered this issue
    violation is being treated as an NCV, consistent with Section VI.A of the NRC
into its CAP as CRs 03-02577, 03-06901, and 03-07256. Because this violation was of
    Enforcement Policy. (NCV 05000346/2003010-28)
very low safety significance and because it was entered into the licensees CAP, the
(6) Review of Licensee Event Reports
violation is being treated as an NCV, consistent with Section VI.A of the NRC
a. Inspection Scope
Enforcement Policy. (NCV 05000346/2003010-28)
    The team reviewed the licensees CAP to identify and address problems previously
(6)
    identified and documented in licensee event reports.
Review of Licensee Event Reports
                                            88                                        Enclosure
  a.
Inspection Scope
The team reviewed the licensees CAP to identify and address problems previously
identified and documented in licensee event reports.


b. Findings
Enclosure
.1 (Discussed) LER 05000346/2002-008-00 and -01: Containment Air Coolers
89
    Collective Significance of Degraded Conditions
  b.
    Introduction: The team reviewed this LER which related to the operability of the CACs
Findings
    during previous operating cycles.
    .1
    Description: Following unit shutdown in 2002, various degraded conditions were
(Discussed) LER 05000346/2002-008-00 and -01: Containment Air Coolers
    identified associated with the CACs, which were documented in several CRs. The
Collective Significance of Degraded Conditions
    issues were related to thermal performance degradation, and structural issues
Introduction: The team reviewed this LER which related to the operability of the CACs
    (CR 02-05563) related to seismic adequacy, boric acid corrosion, and post accident
during previous operating cycles.
    thermal stress. Thermal performance issues caused by cooling coil fouling conditions
Description: Following unit shutdown in 2002, various degraded conditions were
    on the air (cooling fin) side, and water (inside tube) side were identified. Additionally,
identified associated with the CACs, which were documented in several CRs. The
    foreign material (plywood) was found in the SW supply piping to CAC # 2. In addition,
issues were related to thermal performance degradation, and structural issues
    two 10 CFR Part 21 reports were issued by the CAC control vendor and the motor
(CR 02-05563) related to seismic adequacy, boric acid corrosion, and post accident
    vendor. The overall corrective action to resolve the physical degradation of the CAC
thermal stress. Thermal performance issues caused by cooling coil fouling conditions
    units was the refurbishment of the units prior to plant restart. New CAC units were
on the air (cooling fin) side, and water (inside tube) side were identified. Additionally,
    installed.
foreign material (plywood) was found in the SW supply piping to CAC # 2. In addition,
    An engineering evaluation was performed to assess the effects of the degraded
two 10 CFR Part 21 reports were issued by the CAC control vendor and the motor
    conditions on heat transfer capability from which past operability was determined. The
vendor. The overall corrective action to resolve the physical degradation of the CAC
    licensee concluded that the effects of the degraded conditions (including foreign
units was the refurbishment of the units prior to plant restart. New CAC units were
    material in the cooling water line) on heat transfer capability of the CACs, when
installed.
    operating in conjunction with the CS system, would not have rendered the CACs
An engineering evaluation was performed to assess the effects of the degraded
    inoperable with respect to the long term post-accident containment heat removal
conditions on heat transfer capability from which past operability was determined. The
    capability. These evaluations included containment pressure reduction, increased sump
licensee concluded that the effects of the degraded conditions (including foreign
    temperature effects on ECCS pumps NPSH, ECCS pump room heatup, equipment
material in the cooling water line) on heat transfer capability of the CACs, when
    environmental qualification, and radiological release. A NCV was identified in Section
operating in conjunction with the CS system, would not have rendered the CACs
    4OA3(3)b.3, for failure to implement effective design control measures to check and
inoperable with respect to the long term post-accident containment heat removal
    verify the adequacy of the design basis calculation performed for offsite dose
capability. These evaluations included containment pressure reduction, increased sump
    consequences of degraded CACs.
temperature effects on ECCS pumps NPSH, ECCS pump room heatup, equipment
    The licensee performed an engineering evaluation of the structural issues and
environmental qualification, and radiological release. A NCV was identified in Section
    concluded that the issues resulted in a degraded condition, but the CACs were not
4OA3(3)b.3, for failure to implement effective design control measures to check and
    rendered inoperable. The licensee stated that, while corrosion and pitting were
verify the adequacy of the design basis calculation performed for offsite dose
    observed, the "as found" condition would not have been sufficiently degraded to prevent
consequences of degraded CACs.
    the CACs from performing as seismically designed.
The licensee performed an engineering evaluation of the structural issues and
    The licensee determined that the station had no safety related parts applicable to the
concluded that the issues resulted in a degraded condition, but the CACs were not
    10 CFR Part 21 notification made by the controls vendor. At the time of receipt of the
rendered inoperable. The licensee stated that, while corrosion and pitting were
    Part 21 notification from the motor vendor, the licensee stated that the plant was in
observed, the "as found" condition would not have been sufficiently degraded to prevent
    Mode 6 and the CAC motors were being refurbished as part of the overall CAC
the CACs from performing as seismically designed.
    refurbishment. The notification reported a deficiency with a stator winding, which could
The licensee determined that the station had no safety related parts applicable to the
    result in motor winding failure. According to the licensee, no winding failures or
10 CFR Part 21 notification made by the controls vendor. At the time of receipt of the
    anomalies were experienced during fan operation.
Part 21 notification from the motor vendor, the licensee stated that the plant was in
    During review of the LER, the team identified several concerns with the licensees
Mode 6 and the CAC motors were being refurbished as part of the overall CAC
    evaluation. For example:
refurbishment. The notification reported a deficiency with a stator winding, which could
                                              89                                      Enclosure
result in motor winding failure. According to the licensee, no winding failures or
anomalies were experienced during fan operation.
During review of the LER, the team identified several concerns with the licensees
evaluation. For example:


*       The licensee stated in the LER that "Since the service conditions for CACs #1
Enclosure
        and #2 are similar to CAC #3, the degraded conditions on CAC #3 were
90
        considered to be representative of the other CAC cooling coils." However, the
*
        team determined that the #3 CAC was normally in standby, with CACs 1 and 2
The licensee stated in the LER that "Since the service conditions for CACs #1
        being in operation. Therefore, the team could not agree that the condition in
and #2 are similar to CAC #3, the degraded conditions on CAC #3 were
        CAC 3 was representative of the condition of the other two CACs.
considered to be representative of the other CAC cooling coils." However, the
*       The licensee noted that "a piece of plywood measuring approximately 5 inches
team determined that the #3 CAC was normally in standby, with CACs 1 and 2
        by 7 inches was discovered in the 8-inch diameter supply line upstream of the
being in operation. Therefore, the team could not agree that the condition in
        transition to two 6-inch pipes, each of which supplies SW to one of two
CAC 3 was representative of the condition of the other two CACs.
        independent cooling coil manifolds." The licensee stated that the presence of
*
        the plywood was believed to be an isolated condition that occurred during RFO
The licensee noted that "a piece of plywood measuring approximately 5 inches
        12 in 2000. However, the licensee did not provide any information as to work
by 7 inches was discovered in the 8-inch diameter supply line upstream of the
        performed during RFO 12 which would have resulted in leaving a piece of
transition to two 6-inch pipes, each of which supplies SW to one of two
        plywood behind. The licensee also noted that there were no intervening pipe
independent cooling coil manifolds." The licensee stated that the presence of
        fittings or valves between the as-found location of the foreign material and the
the plywood was believed to be an isolated condition that occurred during RFO
        two 6-inch transitions; however, the licensee did not provide any further
12 in 2000. However, the licensee did not provide any information as to work
        justification why the SW flow to this CAC would not be disrupted during a design
performed during RFO 12 which would have resulted in leaving a piece of
        basis event.
plywood behind. The licensee also noted that there were no intervening pipe
*       In the thermal performance analysis section the licensee stated that, "Air side
fittings or valves between the as-found location of the foreign material and the
        degradation consisted of boric acid residue and dirt which may impede the heat
two 6-inch transitions; however, the licensee did not provide any further
        transfer characteristic of the cooling fins." However, in the preceding section on
justification why the SW flow to this CAC would not be disrupted during a design
        structural issues, the air side was characterized as having "moderate to severe
basis event.
        corrosion" and noted that "corrosion and pitting" were observed. The licensee
*
        did not explain why the two sections differed, much less explain difference in
In the thermal performance analysis section the licensee stated that, "Air side
        heat transfer characteristic impact from "residue and dirt" to that obtained from
degradation consisted of boric acid residue and dirt which may impede the heat
        "corrosion and pitting."
transfer characteristic of the cooling fins." However, in the preceding section on
*       The LER also stated that, "operation of the CAC units was directly into high fan
structural issues, the air side was characterized as having "moderate to severe
        speed for normal operation." This statement did not address the fact that during
corrosion" and noted that "corrosion and pitting" were observed. The licensee
        response to an accident, the two operating fans would shift from high to low
did not explain why the two sections differed, much less explain difference in
        speed. Shifting from high to low speed was one of the factors mentioned in the
heat transfer characteristic impact from "residue and dirt" to that obtained from
        Part 21 report on the motors as causing motor failures. It also did not mention
"corrosion and pitting."
        that the motor on the normally operating CAC 1 was replaced during a mid-cycle
*
        outage in 1999.
The LER also stated that, "operation of the CAC units was directly into high fan
*       The licensee's conclusion that the effects of the degraded conditions on the heat
speed for normal operation." This statement did not address the fact that during
        transfer capability of the CACs, when operating in conjunction with the CS
response to an accident, the two operating fans would shift from high to low
        system did not address the fact that the CS system was also degraded due to
speed. Shifting from high to low speed was one of the factors mentioned in the
        the previously identified sump issues.
Part 21 report on the motors as causing motor failures. It also did not mention
that the motor on the normally operating CAC 1 was replaced during a mid-cycle
outage in 1999.  
*
The licensee's conclusion that the effects of the degraded conditions on the heat
transfer capability of the CACs, when operating in conjunction with the CS
system did not address the fact that the CS system was also degraded due to
the previously identified sump issues.
During the review of this LER, the team identified additional issues concerning the
During the review of this LER, the team identified additional issues concerning the
original motor sizing calculation and the lack of thermal relief valves on the CAC SW
original motor sizing calculation and the lack of thermal relief valves on the CAC SW
piping inside containment as described in Sections 4OA3(3)b.3. Because of the overall
piping inside containment as described in Sections 4OA3(3)b.3. Because of the overall
deficiencies in the licensee's evaluation, especially in regard to the thermal performance
deficiencies in the licensee's evaluation, especially in regard to the thermal performance
issue, the team was unable to agree with the licensee's conclusion that the CACs were
issue, the team was unable to agree with the licensee's conclusion that the CACs were
operable during previous cycles.
operable during previous cycles.
                                          90                                      Enclosure


  The team determined that this LER will remain open pending further review of the CAC
Enclosure
  degradation; specifically the extent of degradation and effect on the safety function of
91
  the CACs. For this particular LER, the additional reviews will provide information as to
The team determined that this LER will remain open pending further review of the CAC
  the ability of the CACs to provide cooling for the PORVs during feed and bleed
degradation; specifically the extent of degradation and effect on the safety function of
  operations. The LER will remain open pending resolution of this issue.
the CACs. For this particular LER, the additional reviews will provide information as to
.2 (Closed) LER 05000346/2002-009-00: Degradation of the High Pressure
the ability of the CACs to provide cooling for the PORVs during feed and bleed
  Injection Thermal Sleeves
operations. The LER will remain open pending resolution of this issue.
  On November 29, 2002, with the reactor defueled, it was discovered that the thermal
    .2
  sleeve connected to the 2-2 HPI /makeup nozzle had an axial crack. Inspection of the
(Closed) LER 05000346/2002-009-00: Degradation of the High Pressure
  2-1 HPI/makeup thermal sleeve also revealed a cracked thermal sleeve. No cracking
Injection Thermal Sleeves
  was observed during the inspection of the remaining two HPI thermal sleeves. The
On November 29, 2002, with the reactor defueled, it was discovered that the thermal
  licensee reported that the nozzles with undamaged thermal sleeves had not been used
sleeve connected to the 2-2 HPI /makeup nozzle had an axial crack. Inspection of the
  for RCS makeup. The licensee determined that the axial cracks identified in the thermal
2-1 HPI/makeup thermal sleeve also revealed a cracked thermal sleeve. No cracking
  sleeves did not affect the ability of the HPI system to perform its design function nor did
was observed during the inspection of the remaining two HPI thermal sleeves. The
  either crack provide a source for RCS pressure boundary leakage. Furthermore, since
licensee reported that the nozzles with undamaged thermal sleeves had not been used
  no loss of material occurred, this condition had no impact on the integrity of the fuel
for RCS makeup. The licensee determined that the axial cracks identified in the thermal
  cladding.
sleeves did not affect the ability of the HPI system to perform its design function nor did
  Upon discovery of the cracks in both thermal sleeves, the sleeves were removed and
either crack provide a source for RCS pressure boundary leakage. Furthermore, since
  new ones were installed. The licensee determined that high cycle thermal fatigue was
no loss of material occurred, this condition had no impact on the integrity of the fuel
  the root cause of the identified cracking. A contributing cause was the rate and
cladding.
  oscillation of makeup flow through the primary makeup nozzle. The licensee stated that
Upon discovery of the cracks in both thermal sleeves, the sleeves were removed and
  the appearance of the cracked sleeves was consistent with cases observed at other
new ones were installed. The licensee determined that high cycle thermal fatigue was
  B&W plants.
the root cause of the identified cracking. A contributing cause was the rate and
  The remedial action was to replace the thermal sleeves. Inservice inspection
oscillation of makeup flow through the primary makeup nozzle. The licensee stated that
  procedures were developed to ensure proper inspection techniques were used in the
the appearance of the cracked sleeves was consistent with cases observed at other
  future to verify the integrity of the HPI/makeup thermal sleeves. The licensee stated
B&W plants.
  that the visual inspections will include the use of high resolution video equipment and
The remedial action was to replace the thermal sleeves. Inservice inspection
  verification that the video equipment was applied in accordance with ASME Section XI,
procedures were developed to ensure proper inspection techniques were used in the
  sub-article IWA 2210, Visual Exam for VT-1 Examination. The licensee stated that the
future to verify the integrity of the HPI/makeup thermal sleeves. The licensee stated
  frequency of inspection would be every other refueling outage. This issue was entered
that the visual inspections will include the use of high resolution video equipment and
  into the licensees CAP as CRs 02-09739, 02-9928, and 03-02445.
verification that the video equipment was applied in accordance with ASME Section XI,
  The team reviewed the licensee's corrective actions and determined them to be
sub-article IWA 2210, Visual Exam for VT-1 Examination. The licensee stated that the
  acceptable. No violation of regulatory requirements was identified. This item is closed.
frequency of inspection would be every other refueling outage. This issue was entered
.3 (Closed) LER 05000346/2003-003-00 and -01: Potential Inadequate High
into the licensees CAP as CRs 02-09739, 02-9928, and 03-02445.
  Pressure Injection Pump Minimum Recirculation Flow Following a Small Break
The team reviewed the licensee's corrective actions and determined them to be
  Loss of Coolant Accident
acceptable. No violation of regulatory requirements was identified. This item is closed.
  Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
    .3
  having very low safety significance (Green). Specifically, the licensee failed to provide
(Closed) LER 05000346/2003-003-00 and -01: Potential Inadequate High
  for the original plant design to incorporate a safety-related recirculation path for the HPI
Pressure Injection Pump Minimum Recirculation Flow Following a Small Break
  pumps in the HPR mode of operation. Following discovery, the licensee entered the
Loss of Coolant Accident
  issue into its corrective action process.
Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,
                                              91                                      Enclosure
having very low safety significance (Green). Specifically, the licensee failed to provide
for the original plant design to incorporate a safety-related recirculation path for the HPI
pumps in the HPR mode of operation. Following discovery, the licensee entered the
issue into its corrective action process.


Description: Following the questioning during the 2002 NRC SSDI inspection of a
Enclosure
92
Description: Following the questioning during the 2002 NRC SSDI inspection of a
potential deadhead condition of the HPI pumps and the adequacy of thermal protection
potential deadhead condition of the HPI pumps and the adequacy of thermal protection
(minimum flow) for the pumps, the licensee performed a study, 86-5022260-00, to
(minimum flow) for the pumps, the licensee performed a study, 86-5022260-00, to
Line 4,550: Line 5,012:
transition area) to 0.0045 ft2, which would result in RCS re-pressurization cycles that
transition area) to 0.0045 ft2, which would result in RCS re-pressurization cycles that
could continue following HPI pump realignment to the containment emergency sump
could continue following HPI pump realignment to the containment emergency sump
and closure of the minimum flow recirculation valves. The study concluded that for this
and closure of the minimum flow recirculation valves. The study concluded that for this
newly analyzed range of break sizes, past operability of the HPI pumps was a concern.
newly analyzed range of break sizes, past operability of the HPI pumps was a concern.  
This was because the re-pressurization cycles would result in a higher RCS pressure
This was because the re-pressurization cycles would result in a higher RCS pressure
than the shut-off head of the HPI pumps, resulting in pump dead heading (no flow),
than the shut-off head of the HPI pumps, resulting in pump dead heading (no flow),
when HPI pump suction was from the sump. The licensee documented this condition in
when HPI pump suction was from the sump. The licensee documented this condition in
CR 02-06702 and LER 05000346/2003-003. The condition existed since the original
CR 02-06702 and LER 05000346/2003-003. The condition existed since the original
design of Davis-Besse. The NRC had previously highlighted the potential for this
design of Davis-Besse. The NRC had previously highlighted the potential for this
concern as part of Information Notice (IN) 85-94.
concern as part of Information Notice (IN) 85-94.
Based on the results of the evaluation, several corrective actions were implemented. An
Based on the results of the evaluation, several corrective actions were implemented. An
additional minimum flow recirculation line was installed during RFO 13 for each HPI
additional minimum flow recirculation line was installed during RFO 13 for each HPI
pump. For one pump, the line tapped off the previously existing minimum flow line and
pump. For one pump, the line tapped off the previously existing minimum flow line and
for the other a completely new recirculation line was installed. For both pumps, the new
for the other a completely new recirculation line was installed. For both pumps, the new
lines contained two isolation valves and a non-cavitating pressure breakdown orifice and
lines contained two isolation valves and a non-cavitating pressure breakdown orifice and
connected to the low pressure injection (LPI) pump discharge upstream of its respective
connected to the low pressure injection (LPI) pump discharge upstream of its respective
decay heat cooler for the corresponding safety train. These additional recirculation lines
decay heat cooler for the corresponding safety train. These additional recirculation lines
were designed to provide the original minimum flow protection of the HPI pumps,
were designed to provide the original minimum flow protection of the HPI pumps,  
35 gpm, when aligned to the emergency sump in "piggyback" operation with the DHR
35 gpm, when aligned to the emergency sump in "piggyback" operation with the DHR
pumps. In this lineup, the decay heat coolers would provide cooling for the respective
pumps. In this lineup, the decay heat coolers would provide cooling for the respective
HPI Pumps without loss of sump inventory.
HPI Pumps without loss of sump inventory.
Operator action would be required to open the valves on these additional recirculation
Operator action would be required to open the valves on these additional recirculation
lines prior to pump realignment from the BWST to the emergency sump. Because the
lines prior to pump realignment from the BWST to the emergency sump. Because the
postulated transient was a very slow developing scenario, the team determined that
postulated transient was a very slow developing scenario, the team determined that
ample time would be available for operators to take this action. Additionally, the team
ample time would be available for operators to take this action. Additionally, the team
confirmed that this action did not replace any existing automatic action. The licensee
confirmed that this action did not replace any existing automatic action. The licensee
revised the emergency procedures to provide direction on establishing the HPI alternate
revised the emergency procedures to provide direction on establishing the HPI alternate
minimum recirculation flowpath and provided training to the operators on its use.
minimum recirculation flowpath and provided training to the operators on its use.
These corrective actions were deemed to be sufficient to resolve the concern addressed
These corrective actions were deemed to be sufficient to resolve the concern addressed
in the LER. See Section 4OA3(3)b.1, for further discussion regarding the adequacy of
in the LER. See Section 4OA3(3)b.1, for further discussion regarding the adequacy of
the 35 gpm minimum recirculation flow.
the 35 gpm minimum recirculation flow.
Analysis: The team determined that a performance deficiency existed because the
Analysis: The team determined that a performance deficiency existed because the
original design did not incorporate a safety-related recirculation path for the HPI pumps
original design did not incorporate a safety-related recirculation path for the HPI pumps
in the high pressure recirculation (HPR) mode of operation. Since there was a
in the high pressure recirculation (HPR) mode of operation. Since there was a
performance deficiency, the team compared this performance deficiency to the minor
performance deficiency, the team compared this performance deficiency to the minor
questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor
Inspection Reports." The team concluded that the issue was more than minor because
Inspection Reports." The team concluded that the issue was more than minor because
the licensee failed to provide for the original plant design to incorporate a safety-related
the licensee failed to provide for the original plant design to incorporate a safety-related
                                          92                                      Enclosure


    recirculation path for the HPI pumps in the HPR mode of operation and this finding
Enclosure
    affected the mitigating systems cornerstone. The team reviewed this finding in
93
    accordance with IMC 0609, "Significance Determination Process.
recirculation path for the HPI pumps in the HPR mode of operation and this finding
    The Region III SRAs, evaluated this issue within Phase 1 of the SDP. Based on the
affected the mitigating systems cornerstone. The team reviewed this finding in
    review, the SRAs determined that the HPR safety-function would not actually have been
accordance with IMC 0609, "Significance Determination Process.
    lost because of reliance on procedure actions for feed and bleed operation of the PORV
The Region III SRAs, evaluated this issue within Phase 1 of the SDP. Based on the
    in situations where the SGs could not be used to remove decay heat. Specifically, for
review, the SRAs determined that the HPR safety-function would not actually have been
    initiating events where RCS leakage was not sufficient to remove decay heat
lost because of reliance on procedure actions for feed and bleed operation of the PORV
    (transients, small LOCAs) the Phase 2 SDP plant specific notebook for Davis-Besse
in situations where the SGs could not be used to remove decay heat. Specifically, for
    takes credit for opening of the non-safety-related PORV to remove decay heat from the
initiating events where RCS leakage was not sufficient to remove decay heat
    RCS. Opening of the PORV would allow sufficient HPR flow to ensure adequate
(transients, small LOCAs) the Phase 2 SDP plant specific notebook for Davis-Besse
    minimum flow to ensure pump cooling. Therefore, the finding screened out as having
takes credit for opening of the non-safety-related PORV to remove decay heat from the
    very low safety significance (Green).
RCS. Opening of the PORV would allow sufficient HPR flow to ensure adequate
    Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
minimum flow to ensure pump cooling. Therefore, the finding screened out as having
    measures be established to assure that applicable regulatory requirements and the
very low safety significance (Green).
    design basis were correctly translated into specifications, drawings, procedures, and
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that
    instructions. Furthermore, it requires that measures be provided for verifying or
measures be established to assure that applicable regulatory requirements and the
    checking the adequacy of design, such as by the performance of design reviews, by the
design basis were correctly translated into specifications, drawings, procedures, and
    use of alternate or simplified calculational methods, or by the performance of a suitable
instructions. Furthermore, it requires that measures be provided for verifying or
    testing program.
checking the adequacy of design, such as by the performance of design reviews, by the
    Contrary to the above, the licensee failed to provide for the original plant design to
use of alternate or simplified calculational methods, or by the performance of a suitable
    incorporate a safety-related recirculation path for the HPI pumps in the HPR mode of
testing program.
    operation. The licensee documented this condition in CR 02-06702. These corrective
Contrary to the above, the licensee failed to provide for the original plant design to
    actions were deemed to be sufficient to resolve the concern addressed in the LER.
incorporate a safety-related recirculation path for the HPI pumps in the HPR mode of
    Since the issue was of very low safety significance and was captured in the licensee's
operation. The licensee documented this condition in CR 02-06702. These corrective
    CR, it is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement
actions were deemed to be sufficient to resolve the concern addressed in the LER.  
    Policy. (NCV 05000346/2003010-29)
Since the issue was of very low safety significance and was captured in the licensee's
CR, it is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement
Policy. (NCV 05000346/2003010-29)
4OA4 Cross-Cutting Aspects of Findings
4OA4 Cross-Cutting Aspects of Findings
    The teams findings and observations, as documented in this report, revealed numerous
The teams findings and observations, as documented in this report, revealed numerous
    examples where the licensees corrective action program exhibited implementation
examples where the licensees corrective action program exhibited implementation
    weaknesses and a general lack of engineering rigor in the conduct of engineering
weaknesses and a general lack of engineering rigor in the conduct of engineering
    activities. These concerns further represent deficiencies relating to the cross-cutting
activities. These concerns further represent deficiencies relating to the cross-cutting
    areas of human performance and corrective actions. Specific deficiencies and concerns
areas of human performance and corrective actions. Specific deficiencies and concerns
    supporting this conclusion are documented in sections listed below.
supporting this conclusion are documented in sections listed below.
    Findings Affecting Human Performance
Findings Affecting Human Performance
    4OA3(2)b.2     Lack of 480 Vac Class 1E Motor Thermal Overload Protection
4OA3(2)b.2
    4OA3(3)b.6     Non-conservative Calculation Used in Design Analysis to Determine
Lack of 480 Vac Class 1E Motor Thermal Overload Protection
                    Required Service Water Makeup Flow to Component Cooling Water
4OA3(3)b.6
    4OA3(3)b.11 Service Water Discharge Path Swapover Setpoint
Non-conservative Calculation Used in Design Analysis to Determine
    4OA3(3)b.12 Service Water Discharge Check Valve Test Acceptance Criteria
Required Service Water Makeup Flow to Component Cooling Water
    4OA3(3)b.14 Auxiliary Feedwater System Calculation Issues With Main Steam Safety
4OA3(3)b.11 Service Water Discharge Path Swapover Setpoint
                    Valves
4OA3(3)b.12 Service Water Discharge Check Valve Test Acceptance Criteria
                                              93                                      Enclosure
4OA3(3)b.14 Auxiliary Feedwater System Calculation Issues With Main Steam Safety
Valves


      4OA3(3)b.21 Environmental Qualification of Equipment Not Supported by Analysis
Enclosure
      4OA3(3)b.23 Inappropriate Application of 10 CFR 50.59
94
      4OA3(4)b         Repetitive Spacer Grid Strap Damage
4OA3(3)b.21 Environmental Qualification of Equipment Not Supported by Analysis
      Findings Affecting Corrective Action Program
4OA3(3)b.23 Inappropriate Application of 10 CFR 50.59
      4OA3(2)b.3       Failure to Perform Adequate Direct Current Contactor Testing to Ensure
4OA3(4)b
                      Minimum Voltage at Motor Operated Valves
Repetitive Spacer Grid Strap Damage
      4OA3(2)b.4       Failure to Verify Adequacy of Short Circuit Protection for Direct
Findings Affecting Corrective Action Program
                      Current Circuits
4OA3(2)b.3
      4OA3(2)b.5       Lack of Calculations to Ensure Minimum Voltage Availability at
Failure to Perform Adequate Direct Current Contactor Testing to Ensure
                      Device Terminals
Minimum Voltage at Motor Operated Valves
      4OA3(3)b.1       High Pressure Injection Pump Operation Under Long Term Minimum
4OA3(2)b.4
                      Flow
Failure to Verify Adequacy of Short Circuit Protection for Direct
      4OA3(3)b.2       Increased Dose Consequences Due to Degraded Thermal Performance
Current Circuits
                      Operation of Degraded Containment Air Coolers
4OA3(2)b.5
      4OA3(3)b.3       Containment Air Cooler Air Flow Calculation Concerns
Lack of Calculations to Ensure Minimum Voltage Availability at
      4OA3(3)b.7       Calculation Concerns for Service Water Pump Room Ventilation System
Device Terminals
      4OA3(3)b.11     Service Water Discharge Path Swapover Setpoint
4OA3(3)b.1
      4OA3(3)b.12     Service Water Discharge Check Valve Test Acceptance Criteria
High Pressure Injection Pump Operation Under Long Term Minimum
      4OA3(3)b.13     Lack of Design Basis Calculations to Support Service Water Single
Flow
                      Failure Assumptions
4OA3(3)b.2
      4OA3(3)b.15     Auxiliary Feedwater Strainer Mesh Size and Preconditioning of Auxiliary
Increased Dose Consequences Due to Degraded Thermal Performance
                      Feedwater System During Testing
Operation of Degraded Containment Air Coolers
      4OA3(3)b.19     Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover Stud
4OA3(3)b.3
                      Overstressing
Containment Air Cooler Air Flow Calculation Concerns
      4OA3(4)b         Repetitive Spacer Grid Strap Damage
4OA3(3)b.7
      4OA3.(5)b.1     Process Monitoring Function for Alternative Shutdown Capability
Calculation Concerns for Service Water Pump Room Ventilation System
      4OA3.(5)b.2     Supporting Functions for Alternative Shutdown Capability
4OA3(3)b.11 Service Water Discharge Path Swapover Setpoint
4OA3(3)b.12 Service Water Discharge Check Valve Test Acceptance Criteria
4OA3(3)b.13 Lack of Design Basis Calculations to Support Service Water Single
Failure Assumptions
4OA3(3)b.15 Auxiliary Feedwater Strainer Mesh Size and Preconditioning of Auxiliary
Feedwater System During Testing
4OA3(3)b.19 Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover Stud
Overstressing
4OA3(4)b
Repetitive Spacer Grid Strap Damage
4OA3.(5)b.1
Process Monitoring Function for Alternative Shutdown Capability
4OA3.(5)b.2
Supporting Functions for Alternative Shutdown Capability
4OA5 Other Activities
4OA5 Other Activities
(1)   Assessment of the Licensees Corrective Actions to Address Previously Identified
(1)
      Findings Documented in NRC Reports
Assessment of the Licensees Corrective Actions to Address Previously Identified
   a. Inspection Scope
Findings Documented in NRC Reports
      The team conducted a review of previously identified items to determine effectiveness of
   a.
      identification, evaluation and resolution of issues.
Inspection Scope
   b. Findings
The team conducted a review of previously identified items to determine effectiveness of
.1   Follow up on Findings Documented in Report 05000346/2002012
identification, evaluation and resolution of issues.
  .1 (Closed) URI 05000346/2002012-02: Potential Impact of Corrosion on the
   b.
      Ground Function of Electrical Conduit in Containment
Findings
      During a previous inspection conducted in October 2002, the NRC team noted that
.1
      corrosion appeared to be particularly concentrated in areas where moisture and boric
Follow up on Findings Documented in Report 05000346/2002012
                                                94                                      Enclosure
    .1
(Closed) URI 05000346/2002012-02: Potential Impact of Corrosion on the
Ground Function of Electrical Conduit in Containment
During a previous inspection conducted in October 2002, the NRC team noted that
corrosion appeared to be particularly concentrated in areas where moisture and boric


      acid from the containment atmosphere had condensed and dripped onto electrical
Enclosure
      components. In particular, the NRC team noted substantial corrosion and deposits of
95
      crystallized boric acid on conduits. Based on this observation, the NRC team identified
acid from the containment atmosphere had condensed and dripped onto electrical
      a concern that boric acid corrosion of conduit may create a high electrical resistence
components. In particular, the NRC team noted substantial corrosion and deposits of
      and challenge the ground function of the electrical conduit.
crystallized boric acid on conduits. Based on this observation, the NRC team identified
      This condition was documented by the licensee in CR 02-06788. The CR described a
a concern that boric acid corrosion of conduit may create a high electrical resistence
      condition where boric acid corrosion of conduits in the containment could inhibit the flow
and challenge the ground function of the electrical conduit.
      of ground fault currents through the conduits (conduits provide a supplementary
This condition was documented by the licensee in CR 02-06788. The CR described a
      grounding path for smaller motors).
condition where boric acid corrosion of conduits in the containment could inhibit the flow
      The cause analysis for CR 02-06788 determined that, as a general rule, up to 50
of ground fault currents through the conduits (conduits provide a supplementary
      percent loss of conduit cross sectional area was acceptable without loss of function as
grounding path for smaller motors).
      an electrical ground path. The conduits in question were determined to have only
The cause analysis for CR 02-06788 determined that, as a general rule, up to 50
      surface corrosion amounting to less than 25 percent reduction in cross sectional area
percent loss of conduit cross sectional area was acceptable without loss of function as
      and were therefore, deemed acceptable.
an electrical ground path. The conduits in question were determined to have only
      Subsequently, CR 03-05239 was issued stating that no loss in wall thickness was
surface corrosion amounting to less than 25 percent reduction in cross sectional area
      acceptable for1/2-inch and 3/4-inch conduits. Ultrasonic testing was performed to
and were therefore, deemed acceptable.
      determine the wall thickness of corroded conduits; however, no decision had been made
Subsequently, CR 03-05239 was issued stating that no loss in wall thickness was
      as to resolution of this issue. Following questions by the team, the licensee determined
acceptable for1/2-inch and 3/4-inch conduits. Ultrasonic testing was performed to
      that all conduits were acceptable as-is. Based on this conclusion, the team determined
determine the wall thickness of corroded conduits; however, no decision had been made
      that no violation of NRC requirements existed. This URI is considered closed.
as to resolution of this issue. Following questions by the team, the licensee determined
  .2 (Closed) URI 05000346/2002012-03: Potential Failure to Follow the Procedure
that all conduits were acceptable as-is. Based on this conclusion, the team determined
      for Raychem' Splice Removal on Electrical Cables
that no violation of NRC requirements existed. This URI is considered closed.
      During CAC motor replacement, the licensee identified splitting of the motor cable
    .2
      insulation as documented in CR 02-05459. The resolution of this issue is discussed in
(Closed) URI 05000346/2002012-03: Potential Failure to Follow the Procedure
      Section 4OA3(2)b.6. The URI is closed.
for Raychem' Splice Removal on Electrical Cables
.2   Follow-up on SSDI Findings Documented in Report 05000346/2002014
During CAC motor replacement, the licensee identified splitting of the motor cable
  .1 (Discussed) NCV 05000346/2002014-01a: Lack of a Design Basis Analysis for
insulation as documented in CR 02-05459. The resolution of this issue is discussed in
      Containment Isolation Valve Backup Air Supplies
Section 4OA3(2)b.6. The URI is closed.
      This violation was written to document an issue regarding the CAC outlet SW valves
.2
      reliance on the availability of the non-seismic instrument air system to maintain pressure
Follow-up on SSDI Findings Documented in Report 05000346/2002014
      on the air operated valves so that they could perform their containment isolation function
    .1
      to remain closed. The resolution of this issue is discussed in Section 4OA3(3)b.4.
(Discussed) NCV 05000346/2002014-01a: Lack of a Design Basis Analysis for
  .2 (Discussed) NCV 05000346/2002014-01b: Inadequate Blowdown Provisions for
Containment Isolation Valve Backup Air Supplies
      Containment Air Cooler Backup Air Accumulators
This violation was written to document an issue regarding the CAC outlet SW valves
      This violation was written to document that there was no provisions to blow down the
reliance on the availability of the non-seismic instrument air system to maintain pressure
      CACs to remove excessive moisture as required by the USAR. The acceptability of the
on the air operated valves so that they could perform their containment isolation function
      corrective actions to this issue is discussed in Section 4OA3(3)b.5.
to remain closed. The resolution of this issue is discussed in Section 4OA3(3)b.4.
                                                95                                    Enclosure
    .2
(Discussed) NCV 05000346/2002014-01b: Inadequate Blowdown Provisions for
Containment Air Cooler Backup Air Accumulators
This violation was written to document that there was no provisions to blow down the
CACs to remove excessive moisture as required by the USAR. The acceptability of the
corrective actions to this issue is discussed in Section 4OA3(3)b.5.


.3 (Closed) URI 05000346/2002014-01c: Failure to Perform Comprehensive
Enclosure
  Moderate Energy Line Break Analysis
96
  This item dealt with the licensees failure to perform a comprehensive moderate energy
    .3
  line break analysis. The resolution of this issue is discussed in Section 4OA3(3)b.24.
(Closed) URI 05000346/2002014-01c: Failure to Perform Comprehensive
  The URI is closed.
Moderate Energy Line Break Analysis
.4 (Closed) URI 05000346/2002014-01d: Lifting of Service Water Relief Valves
This item dealt with the licensees failure to perform a comprehensive moderate energy
  This URI dealt with a continuing operating condition when the relief valves on the tube
line break analysis. The resolution of this issue is discussed in Section 4OA3(3)b.24.  
  (SW) side of the CCW heat exchangers would open when the licensee changed which
The URI is closed.
  pump was operating under low flow conditions such as winter operation with low heat
    .4
  loads. The licensee resolved the problem of inadvertent openings by changing the
(Closed) URI 05000346/2002014-01d: Lifting of Service Water Relief Valves
  operating procedures. The team concluded that relief valve lifting was not a concern
This URI dealt with a continuing operating condition when the relief valves on the tube
  during a design basis event because there would be an increased heat load. This would
(SW) side of the CCW heat exchangers would open when the licensee changed which
  prevent the underlying pressure surge from occurring. No violation of NRC
pump was operating under low flow conditions such as winter operation with low heat
  requirements was identified. This item is closed.
loads. The licensee resolved the problem of inadvertent openings by changing the
.5 (Closed) URI 05000346/2002014-01e: Inadequate Service Water Pump Room
operating procedures. The team concluded that relief valve lifting was not a concern
  Temperature Analysis
during a design basis event because there would be an increased heat load. This would
  This URI concerned non-conservatisms in the analysis which analyzed the heat loads in
prevent the underlying pressure surge from occurring. No violation of NRC
  the SW pump room and the ability of the ventilation system to maintain the pump room
requirements was identified. This item is closed.
  temperatures within a required operating range. The resolution of this issue is
    .5
  discussed in Section 4OA3(3)b.7. The URI is closed.
(Closed) URI 05000346/2002014-01e: Inadequate Service Water Pump Room
.6 (Closed) URI 05000346/2002014-01f: Inadequate Service Water Pump Room
Temperature Analysis
  Steam Line Break Analysis
This URI concerned non-conservatisms in the analysis which analyzed the heat loads in
  This item dealt with the effects of a postulated auxiliary steam line break in the SW
the SW pump room and the ability of the ventilation system to maintain the pump room
  pump room and whether the licensee correctly translated the USAR commitments
temperatures within a required operating range. The resolution of this issue is
  regarding the SW pump room environmental limits into analyses that demonstrated
discussed in Section 4OA3(3)b.7. The URI is closed.
  these limits would not be violated for design basis conditions. This issue is discussed in
    .6
  Section 4OA3(3)b.7. The URI is closed.
(Closed) URI 05000346/2002014-01f: Inadequate Service Water Pump Room
.7 (Closed) URI 05000346/2002014-01g: Inadequate Cable Ampacity Analysis
Steam Line Break Analysis
  On September 24, 2002, the licensee issued CR 02-06893 to document an increase
This item dealt with the effects of a postulated auxiliary steam line break in the SW
  from 95EF to 124EF in Rooms 105 and 115 temperature as a result of an increase of
pump room and whether the licensee correctly translated the USAR commitments
  SW temperature. The CR identified the need to reevaluate cable ampacity as a result of
regarding the SW pump room environmental limits into analyses that demonstrated
  the higher room temperature. The team discussed the ampacity issue with the licensee,
these limits would not be violated for design basis conditions. This issue is discussed in
  and determined there actually was not an ampacity concern. Therefore, this item is
Section 4OA3(3)b.7. The URI is closed.
  considered closed.
    .7
                                            96                                      Enclosure
(Closed) URI 05000346/2002014-01g: Inadequate Cable Ampacity Analysis
On September 24, 2002, the licensee issued CR 02-06893 to document an increase
from 95F to 124F in Rooms 105 and 115 temperature as a result of an increase of
SW temperature. The CR identified the need to reevaluate cable ampacity as a result of
the higher room temperature. The team discussed the ampacity issue with the licensee,
and determined there actually was not an ampacity concern. Therefore, this item is
considered closed.


.8 (Closed) URI 05000346/2002014-01h: Inadequate Flooding Protection for
Enclosure
    Service Water Pump House
97
    This URI dealt with deficiencies in correctly implementing USAR commitments regarding
    .8
    flood protection for the SW pump room. The resolution of this issue is discussed in
(Closed) URI 05000346/2002014-01h: Inadequate Flooding Protection for
    Section 4OA3(3)b.9. The URI is closed.
Service Water Pump House
.9 (Discussed) NCV 05000346/2002014-01i: Non-conservative Technical
This URI dealt with deficiencies in correctly implementing USAR commitments regarding
    Specification Value for 90 Percent Undervoltage Relays
flood protection for the SW pump room. The resolution of this issue is discussed in
    The licensee initiated CR 02-07766 to address the issue that the trip set point specified
Section 4OA3(3)b.9. The URI is closed.
    in calculation C-EE-004.01-049 was greater than the TS allowable value shown in Table
    .9
    3.3-4. Therefore, the postulated TS allowable value could be violated for plant operating
(Discussed) NCV 05000346/2002014-01i: Non-conservative Technical
    conditions where the voltage was just above the relay set point value. The team
Specification Value for 90 Percent Undervoltage Relays
    reviewed the issue and determined that the new calculation, C-EE-015.03-008, which
The licensee initiated CR 02-07766 to address the issue that the trip set point specified
    utilized the ETAP program, properly addressed all issues included in the CR. Therefore,
in calculation C-EE-004.01-049 was greater than the TS allowable value shown in Table
    the corrective actions to this issue were deemed acceptable. Another issue related to
3.3-4. Therefore, the postulated TS allowable value could be violated for plant operating
    allowable values is discussed in Section 4OA3(2)b.1.
conditions where the voltage was just above the relay set point value. The team
.10 (Closed) URI 05000346/2002014-01j: Poor Quality Calculation for 90 Percent
reviewed the issue and determined that the new calculation, C-EE-015.03-008, which
    Undervoltage Relays
utilized the ETAP program, properly addressed all issues included in the CR. Therefore,
    The licensee entered the issue into its CAP as CR 02-07633 which subsequently was
the corrective actions to this issue were deemed acceptable. Another issue related to
    rolled over to CR 02-07646. In order to resolve the concern, the licensee performed a
allowable values is discussed in Section 4OA3(2)b.1.
    new calculation, C-EE-015.03-008, to address this and other electrical issues. Review
    .10 (Closed) URI 05000346/2002014-01j: Poor Quality Calculation for 90 Percent
    of the calculation is discussed in Sections 4OA3(2)b.7 and 4OA5(1)b.2.11. This item is
Undervoltage Relays
    closed.
The licensee entered the issue into its CAP as CR 02-07633 which subsequently was
.11 (Discussed) NCV 05000346/2002014-01k: Non-conservative Relay Setpoint
rolled over to CR 02-07646. In order to resolve the concern, the licensee performed a
    Calculation for the 59 Percent Undervoltage Relays
new calculation, C-EE-015.03-008, to address this and other electrical issues. Review
    The licensee initiated CR 02-06737 and CR 02-07646 to evaluate issues affecting the
of the calculation is discussed in Sections 4OA3(2)b.7 and 4OA5(1)b.2.11. This item is
    relay uncertainty in calculation C-EE-004.01.051. The postulated inconsistencies could
closed.
    have rendered the operation of the 59 percent relay inconsistent with requirements for
    .11 (Discussed) NCV 05000346/2002014-01k: Non-conservative Relay Setpoint
    continuous operation under-voltage transient conditions imposed by the motor inrush
Calculation for the 59 Percent Undervoltage Relays
    current.
The licensee initiated CR 02-06737 and CR 02-07646 to evaluate issues affecting the
    The team reviewed CR 02-07646 and determined that calculation C-EE-015.03-008,
relay uncertainty in calculation C-EE-004.01.051. The postulated inconsistencies could
    which used the ETAP program described in Section 4OA3(2)b.7, had properly
have rendered the operation of the 59 percent relay inconsistent with requirements for
    addressed the postulated inconsistencies and non-conservative assumptions in the
continuous operation under-voltage transient conditions imposed by the motor inrush
    uncertainty analysis. Therefore, the corrective actions to this issue were deemed
current.
    acceptable.
The team reviewed CR 02-07646 and determined that calculation C-EE-015.03-008,
                                            97                                    Enclosure
which used the ETAP program described in Section 4OA3(2)b.7, had properly
addressed the postulated inconsistencies and non-conservative assumptions in the
uncertainty analysis. Therefore, the corrective actions to this issue were deemed
acceptable.


.12 (Closed) URI 05000346/2002014-01l: Inadequate Calculations for Control Room
Enclosure
    Operator Dose (GDC-19) and Offsite Dose (10 CFR Part 100) Related to High
98
    Pressure Injection Pump Minimum Flow Values
    .12 (Closed) URI 05000346/2002014-01l: Inadequate Calculations for Control Room
    This URI addressed concerns with the dose calculations for operators and the general
Operator Dose (GDC-19) and Offsite Dose (10 CFR Part 100) Related to High
    public following a design basis accident. The resolution of this issue is discussed in
Pressure Injection Pump Minimum Flow Values
    Section 4OA3(3)b.18. The URI is closed.
This URI addressed concerns with the dose calculations for operators and the general
.13 (Closed) URI 05000346/2002014-01m: Other GDC-19 and 10 CFR Part 100
public following a design basis accident. The resolution of this issue is discussed in
    Issues
Section 4OA3(3)b.18. The URI is closed.
    This URI addressed concerns with the dose calculations for operators and the general
    .13 (Closed) URI 05000346/2002014-01m: Other GDC-19 and 10 CFR Part 100
    public following a design basis accident. The resolution of this issue is discussed in
Issues
    Section 4OA3(3)b.18. The URI is closed.
This URI addressed concerns with the dose calculations for operators and the general
.14 (Closed) URI 05000346/2002014-01n: High Pressure Injection Pump Operation
public following a design basis accident. The resolution of this issue is discussed in
    Under Long Term Minimum Flow
Section 4OA3(3)b.18. The URI is closed.
    This item dealt with the ability of the HPI pumps to perform as intended during extended
    .14 (Closed) URI 05000346/2002014-01n: High Pressure Injection Pump Operation
    operation on minimum flow. This issue is discussed in Sections 4OA3(3)b.1 and
Under Long Term Minimum Flow
    4OA3(6)b.2. This URI is closed.
This item dealt with the ability of the HPI pumps to perform as intended during extended
.15 (Closed) URI 05000346/2002014-01o: Some Small Break Loss of Coolant
operation on minimum flow. This issue is discussed in Sections 4OA3(3)b.1 and
    Accident Sizes Not Analyzed
4OA3(6)b.2. This URI is closed.
    This URI addressed concerns with the HPI pump potentially not having a flow path upon
    .15 (Closed) URI 05000346/2002014-01o: Some Small Break Loss of Coolant
    the suction being switched from the BWST to the sump. This issue is discussed in
Accident Sizes Not Analyzed
    Section 4OA3(6)b.3. This URI is closed.
This URI addressed concerns with the HPI pump potentially not having a flow path upon
.16 (Closed) URI 05000346/2002014-01p: Inadequate Service Water System Flow
the suction being switched from the BWST to the sump. This issue is discussed in
    Analyses
Section 4OA3(6)b.3. This URI is closed.
    This URI dealt with deficiencies in the assumptions used in SW system flow
    .16 (Closed) URI 05000346/2002014-01p: Inadequate Service Water System Flow
    calculations. The resolution of this issue is discussed in Section 4OA3(3)b.8. The URI
Analyses
    is closed.
This URI dealt with deficiencies in the assumptions used in SW system flow
.17 (Closed) URI 05000346/2002014-01q: Inadequate Service Water System
calculations. The resolution of this issue is discussed in Section 4OA3(3)b.8. The URI
    Thermal Analyses
is closed.
    This URI dealt with deficiencies in the maximum temperatures used in SW system and
    .17 (Closed) URI 05000346/2002014-01q: Inadequate Service Water System
    ultimate heat sink calculations. The resolution of this issue is discussed in Sections
Thermal Analyses
    4OA3(3)b.8 and 4OA3(3)b.13. The URI is closed.
This URI dealt with deficiencies in the maximum temperatures used in SW system and
.18 (Closed) URI 05000346/2002014-01r: Inadequate Ultimate Heat Sink Inventory
ultimate heat sink calculations. The resolution of this issue is discussed in Sections
    Analysis
4OA3(3)b.8 and 4OA3(3)b.13. The URI is closed.
    This URI dealt with deficiencies in the SW system flow and ultimate heat sink minimum
    .18 (Closed) URI 05000346/2002014-01r: Inadequate Ultimate Heat Sink Inventory
    level calculations. The resolution of this issue is discussed in Sections 4OA3(3)b.8 and
Analysis
    4OA3(3)b.13. The URI is closed.
This URI dealt with deficiencies in the SW system flow and ultimate heat sink minimum
                                              98                                    Enclosure
level calculations. The resolution of this issue is discussed in Sections 4OA3(3)b.8 and
4OA3(3)b.13. The URI is closed.


.19 (Closed) URI 05000346/2002014-01s: No Valid Service Water Pump Net
Enclosure
    Positive Suction Head Analysis
99
    This URI dealt with the licensee not having a calculation which showed that the SW
    .19 (Closed) URI 05000346/2002014-01s: No Valid Service Water Pump Net
    pumps had adequate NPSH under all operating conditions. The resolution of this issue
Positive Suction Head Analysis
    is discussed in Section 4OA3(3)b.8. The URI is closed.
This URI dealt with the licensee not having a calculation which showed that the SW
.20 (Closed) URI 05000346/2002014-01t: Service Water Source Temperature
pumps had adequate NPSH under all operating conditions. The resolution of this issue
    Analysis for Auxiliary Feedwater
is discussed in Section 4OA3(3)b.8. The URI is closed.
    This item dealt with SW source for AFW which had not been analyzed with respect to its
    .20 (Closed) URI 05000346/2002014-01t: Service Water Source Temperature
    potentially higher temperature condition for various design basis events and the possible
Analysis for Auxiliary Feedwater
    impact on the ability of the AFW system to perform its safety function. Such effects
This item dealt with SW source for AFW which had not been analyzed with respect to its
    could include reduced heat absorption capability for AFW injected into the SGs and
potentially higher temperature condition for various design basis events and the possible
    inadequate cooling of AFW lubricating oil. The licensees evaluation concluded that
impact on the ability of the AFW system to perform its safety function. Such effects
    temperature of AFW (seismic event with long term AFW supplied by SW) was lower
could include reduced heat absorption capability for AFW injected into the SGs and
    than the design AFW temperature of 120EF as noted in the system description. In
inadequate cooling of AFW lubricating oil. The licensees evaluation concluded that
    addition, the licensee determined that AFW equipment temperature limits were greater
temperature of AFW (seismic event with long term AFW supplied by SW) was lower
    than 120EF. Therefore, the licensee concluded that there was no discrepant condition.
than the design AFW temperature of 120F as noted in the system description. In
    The team agreed with this assessment. This URI is closed.
addition, the licensee determined that AFW equipment temperature limits were greater
.21 (Closed) URI 05000346/2002014-01u: Inadequate Short Circuit Calculations
than 120F. Therefore, the licensee concluded that there was no discrepant condition.  
    This URI was written to document that the licensee had not considered the worst case
The team agreed with this assessment. This URI is closed.
    grid voltage. The resolution of this issue is discussed in Section 4OA3(2)b.8. The URI
    .21 (Closed) URI 05000346/2002014-01u: Inadequate Short Circuit Calculations
    is closed.
This URI was written to document that the licensee had not considered the worst case
.22 (Discussed) NCV 05000346/2002014-01v: No Analytical Basis for Setpoint to
grid voltage. The resolution of this issue is discussed in Section 4OA3(2)b.8. The URI
    Swap Service Water System Discharge Path
is closed.
    There was no analytical basis for the setpoint used to swap the SW system discharge
    .22 (Discussed) NCV 05000346/2002014-01v: No Analytical Basis for Setpoint to
    path from the normally used, but non-seismic lines, to a seismically qualified path. The
Swap Service Water System Discharge Path
    setpoint for the swapover was 50 psig; however, there was no calculational bases for
There was no analytical basis for the setpoint used to swap the SW system discharge
    this setpoint. The acceptability of the corrective actions to this issue is discussed in
path from the normally used, but non-seismic lines, to a seismically qualified path. The
    Section 4OA3(3)b.11.
setpoint for the swapover was 50 psig; however, there was no calculational bases for
.23 (Discussed) NCV 05000346/2002014-02a: Service Water Surveillance Test Did
this setpoint. The acceptability of the corrective actions to this issue is discussed in
    Not Use Worst Case Values
Section 4OA3(3)b.11.
    This violation addressed the fact that a surveillance test did not demonstrate that
    .23 (Discussed) NCV 05000346/2002014-02a: Service Water Surveillance Test Did
    worst-case post-accident conditions were bounded for the CAC discharge valves in the
Not Use Worst Case Values
    SW system.
This violation addressed the fact that a surveillance test did not demonstrate that
    The licensee was replacing these valves, due to a number of problems with them. The
worst-case post-accident conditions were bounded for the CAC discharge valves in the
    proposed corrective actions appeared to include appropriate acceptance criteria. The
SW system.
    team identified a concern with the original evaluation and corrective action wording in
The licensee was replacing these valves, due to a number of problems with them. The
    CR 02-07781. The NCV writeup mentioned that the licensees procedure did not
proposed corrective actions appeared to include appropriate acceptance criteria. The
    declare the valves inoperable and write a CR if the valves failed the valve closure test.
team identified a concern with the original evaluation and corrective action wording in
    This issue was not originally addressed in the licensees corrective actions. However,
CR 02-07781. The NCV writeup mentioned that the licensees procedure did not
                                            99                                        Enclosure
declare the valves inoperable and write a CR if the valves failed the valve closure test.  
This issue was not originally addressed in the licensees corrective actions. However,


    when it was brought to the licensees attention, appropriate changes were made in the
Enclosure
    procedure to address declaring the valve inoperable and writing CRs when necessary.
100
    In responding to a team request for supporting calculations, the licensee also noted that
when it was brought to the licensees attention, appropriate changes were made in the
    a corrective action for the CR 02-07781 was closed prior to a calculation being reviewed
procedure to address declaring the valve inoperable and writing CRs when necessary.  
    and approved. Other examples where corrective actions were closed prior to the
In responding to a team request for supporting calculations, the licensee also noted that
    calculations being approved are discussed in Sections 4OA3(3)b.17 and 4OA3(3)b.19.
a corrective action for the CR 02-07781 was closed prior to a calculation being reviewed
.24 (Closed) URI 05000346/2002014-02b: Inadequate Service Water Flow Balance
and approved. Other examples where corrective actions were closed prior to the
    Testing
calculations being approved are discussed in Sections 4OA3(3)b.17 and 4OA3(3)b.19.
    This URI was written to document concerns with the flow balance testing for the SW
    .24 (Closed) URI 05000346/2002014-02b: Inadequate Service Water Flow Balance
    system. The resolution of this issue is discussed in Section 4OA3(2)b.10. This URI is
Testing
    closed.
This URI was written to document concerns with the flow balance testing for the SW
.25 (Closed) URI 05000346/2002014-03a: Inappropriate Service Water Pump Curve
system. The resolution of this issue is discussed in Section 4OA3(2)b.10. This URI is
    Allowable Degradation
closed.
    In the 2002 NRC SSDI, the team identified an item associated with prompt corrective
    .25 (Closed) URI 05000346/2002014-03a: Inappropriate Service Water Pump Curve
    action to resolve a the licensee identified condition where the allowable degradation of
Allowable Degradation
    the SW pumps did not match the design basis required flow rate for the SW pumps. In
In the 2002 NRC SSDI, the team identified an item associated with prompt corrective
    particular, the pump curve was allowed to degrade by 7 percent in accordance with IST
action to resolve a the licensee identified condition where the allowable degradation of
    acceptance criteria, without evaluating the required design basis flow requirement.
the SW pumps did not match the design basis required flow rate for the SW pumps. In
    Vendor calculations 02-123 and 02-113 were performed to address all SW hydraulic
particular, the pump curve was allowed to degrade by 7 percent in accordance with IST
    issues. The allowable SW pump degradation was included in the new calculations. The
acceptance criteria, without evaluating the required design basis flow requirement.  
    team did not identify any violation. This URI is closed.
Vendor calculations 02-123 and 02-113 were performed to address all SW hydraulic
.26 (Closed) URI 05000346/2002014-03b: Repetitive Failures of Service Water
issues. The allowable SW pump degradation was included in the new calculations. The
    Relief Valves
team did not identify any violation. This URI is closed.
    This URI, URI 02-14-01d, and URI 02-14-06 all dealt with a continuing operating
    .26 (Closed) URI 05000346/2002014-03b: Repetitive Failures of Service Water
    condition where the relief valves on the tube (SW) side of the CCW heat exchangers
Relief Valves
    were opening under routine operating conditions, were failing due to the frequent
This URI, URI 02-14-01d, and URI 02-14-06 all dealt with a continuing operating
    opening, and to the licensee's stated plans to resolve the problem by removal of the
condition where the relief valves on the tube (SW) side of the CCW heat exchangers
    valves from the system, contrary to the requirements of the ASME Code.
were opening under routine operating conditions, were failing due to the frequent
    At the time of the inspection, the licensee had not yet removed the relief valves;
opening, and to the licensee's stated plans to resolve the problem by removal of the
    therefore, the issues raised by the URI still existed. The licensee had taken a number of
valves from the system, contrary to the requirements of the ASME Code.
    actions to reduce the frequency of undesired relief valve openings, primarily through
At the time of the inspection, the licensee had not yet removed the relief valves;
    changes in the operating procedures. The licensee stated that these procedural
therefore, the issues raised by the URI still existed. The licensee had taken a number of
    changes greatly decreased the times that the valves opened unexpectedly. The
actions to reduce the frequency of undesired relief valve openings, primarily through
    reduction in inadvertent openings also resulted in a reduction of valve failures.
changes in the operating procedures. The licensee stated that these procedural
    The team considered The licensees plans to remove the relief valves to be
changes greatly decreased the times that the valves opened unexpectedly. The
    inappropriate as the team did not believe the ASME Code allowed for the valves to be
reduction in inadvertent openings also resulted in a reduction of valve failures.
    removed. The team reviewed the applicable sections of both ASME Section III (the
The team considered The licensees plans to remove the relief valves to be
    Code section applicable to the SW piping) and ASME Section VIII (the Code section
inappropriate as the team did not believe the ASME Code allowed for the valves to be
    under which the heat exchangers were purchased). Both sections clearly indicated that
removed. The team reviewed the applicable sections of both ASME Section III (the
    overpressure protection was required for any piping where heat was being introduced
Code section applicable to the SW piping) and ASME Section VIII (the Code section
    into the system. As the SW system was the cooling mechanism for the CCW heat
under which the heat exchangers were purchased). Both sections clearly indicated that
                                            100                                      Enclosure
overpressure protection was required for any piping where heat was being introduced
into the system. As the SW system was the cooling mechanism for the CCW heat


    exchangers, heat was being introduced into the system, and overpressure protection
Enclosure
    was required. The team also noted that the licensee had manual valves downstream of
101
    the relief valves on the CCW heat exchangers; another area which was not in strict
exchangers, heat was being introduced into the system, and overpressure protection
    compliance with the Code. Subsequent to the inspection, the licensee informed the
was required. The team also noted that the licensee had manual valves downstream of
    team that a decision had not been made to replace the subject valves. Since the
the relief valves on the CCW heat exchangers; another area which was not in strict
    licensee has not removed the valves from service, this URI is closed.
compliance with the Code. Subsequent to the inspection, the licensee informed the
    The issues regarding URI 50-345/2002014-06 will be addressed in a separate report.
team that a decision had not been made to replace the subject valves. Since the
.27 (Closed) URI 05000346/2002014-03c: Non-conservative Difference in Ultimate
licensee has not removed the valves from service, this URI is closed.
    Heat Sink Temperature Measurements
The issues regarding URI 50-345/2002014-06 will be addressed in a separate report.
    This URI dealt with a potential non-conservative temperature measurement for ultimate
    .27 (Closed) URI 05000346/2002014-03c: Non-conservative Difference in Ultimate
    heat sink temperatures. The concern was that the temperature instrument used to
Heat Sink Temperature Measurements
    measure the ultimate heat sink temperature might not be the most conservative and
This URI dealt with a potential non-conservative temperature measurement for ultimate
    might contain up to 2EF of error, which was not accounted for in the SW design basis
heat sink temperatures. The concern was that the temperature instrument used to
    calculations.
measure the ultimate heat sink temperature might not be the most conservative and
    The licensee performed a test which measured the temperature of the ultimate heat sink
might contain up to 2F of error, which was not accounted for in the SW design basis
    in two different locations - the normal input for the computer point, and a second one
calculations.
    which had been reading higher during the October inspection - using sensitive,
The licensee performed a test which measured the temperature of the ultimate heat sink
    calibrated measuring and test equipment. Based on this test, the licensee determined
in two different locations - the normal input for the computer point, and a second one
    that the two locations were reading the same temperature, at least at the time of the
which had been reading higher during the October inspection - using sensitive,
    test. The licensee also noted that the normal temperature instrument had a much
calibrated measuring and test equipment. Based on this test, the licensee determined
    tighter accuracy band (0.75EF) as compared to the other instrument (3EF) such that,
that the two locations were reading the same temperature, at least at the time of the
    even if the second instrument appeared to be reading higher, it might actually be below
test. The licensee also noted that the normal temperature instrument had a much
    the actual ultimate heat sink temperature.
tighter accuracy band (0.75F) as compared to the other instrument (3F) such that,
    The team determined that the licensees procedures had been revised to incorporate the
even if the second instrument appeared to be reading higher, it might actually be below
    temperature instruments uncertainty calculation results into them, and that the
the actual ultimate heat sink temperature.
    procedures required the plant to take appropriate actions should it appear that the
The team determined that the licensees procedures had been revised to incorporate the
    ultimate heat sink temperature was being approached (such as measuring the
temperature instruments uncertainty calculation results into them, and that the
    temperature locally with sensitive measuring and test equipment). Therefore, the team
procedures required the plant to take appropriate actions should it appear that the
    determined that no violation existed. This URI is closed.
ultimate heat sink temperature was being approached (such as measuring the
.28 (Discussed) NCV 05000346/2002014-03d: Inadequate Corrective Actions
temperature locally with sensitive measuring and test equipment). Therefore, the team
    Related to Service Water Pump Discharge Check Valve Acceptance Criteria
determined that no violation existed. This URI is closed.
    This violation addressed an inadequate corrective action in that the acceptance criterion
    .28 (Discussed) NCV 05000346/2002014-03d: Inadequate Corrective Actions
    for the inservice full flow test for the SW pump discharge check valves was determined
Related to Service Water Pump Discharge Check Valve Acceptance Criteria
    to be non-conservative, was corrected, and the new value was still not the full design
This violation addressed an inadequate corrective action in that the acceptance criterion
    flow rate. The acceptability of the corrective actions to this issue is discussed in Section
for the inservice full flow test for the SW pump discharge check valves was determined
    4OA3(2)b.12.
to be non-conservative, was corrected, and the new value was still not the full design
.29 (Closed) URI 05000346/2002014-03e: Non-conservative Containment Air
flow rate. The acceptability of the corrective actions to this issue is discussed in Section
    Cooler Mechanical Stress Analysis
4OA3(2)b.12.
    This item dealt with overestimation of nozzle flexibility by a factor of one thousand when
    .29 (Closed) URI 05000346/2002014-03e: Non-conservative Containment Air
    analyzing the connection of the SW system to the CACs. This item was also briefly
Cooler Mechanical Stress Analysis
    discussed in the section for LER 05000346/2002-008-00 and -01.
This item dealt with overestimation of nozzle flexibility by a factor of one thousand when
                                              101                                      Enclosure
analyzing the connection of the SW system to the CACs. This item was also briefly
discussed in the section for LER 05000346/2002-008-00 and -01.


      Stress analyses concluded that the CACs were operable in the past regarding structural
Enclosure
      concerns identified in CR 02-05563. The structural report concluded that, "...Based on
102
      the lack of significance or the continued structural acceptability identified with the
Stress analyses concluded that the CACs were operable in the past regarding structural
      numerous finding associated with the CAC coil modules and their support structure, the
concerns identified in CR 02-05563. The structural report concluded that, "...Based on
      CAC operability assessment is considered to be unaffected by the composite findings of
the lack of significance or the continued structural acceptability identified with the
      all currently identified, structural-related CAC concerns. The team determined that the
numerous finding associated with the CAC coil modules and their support structure, the
      licensee appropriately used ASME Code F stress criteria in the structural analysis. This
CAC operability assessment is considered to be unaffected by the composite findings of
      item is closed.
all currently identified, structural-related CAC concerns. The team determined that the
  .30 (Discussed) NCV 05000346/2002014-04: Failure to Perform Technical
licensee appropriately used ASME Code F stress criteria in the structural analysis. This
      Specification Surveillance for High Pressure Injection Pump Following
item is closed.
      Maintenance
    .30 (Discussed) NCV 05000346/2002014-04: Failure to Perform Technical
      This item dealt with the failure to perform a surveillance in accordance with TS 4.5.2.H
Specification Surveillance for High Pressure Injection Pump Following
      for HPI pump following maintenance. This TS could not be directly verified by test since
Maintenance
      system pressure could not be easily held at 400 pounds per square inch, absolute
This item dealt with the failure to perform a surveillance in accordance with TS 4.5.2.H
      during full HPI injection. The licensee requested a TS amendment (No. 256) to relocate
for HPI pump following maintenance. This TS could not be directly verified by test since
      the surveillance requirement pertaining to flow balance testing of the HPI and LPI
system pressure could not be easily held at 400 pounds per square inch, absolute  
      subsystems following system modifications to the technical requirement manual. Also,
during full HPI injection. The licensee requested a TS amendment (No. 256) to relocate
      the amendment added ECCS pump operability conditions to the TS. The new
the surveillance requirement pertaining to flow balance testing of the HPI and LPI
      surveillance requirement would require verifying each ECCS pumps developed head to
subsystems following system modifications to the technical requirement manual. Also,
      be greater than or equal to the required developed head, when tested pursuant to TS
the amendment added ECCS pump operability conditions to the TS. The new
      4.0.5 with regards to inservice testing requirements of the ASME Code. The team had
surveillance requirement would require verifying each ECCS pumps developed head to
      no further concerns and did not identify other new issues.
be greater than or equal to the required developed head, when tested pursuant to TS
  .31 (Closed) URI 05000346/2002014-05: Question Regarding Definition of a
4.0.5 with regards to inservice testing requirements of the ASME Code. The team had
      Passive Failure
no further concerns and did not identify other new issues.
      This URI dealt with the question on whether stem-to-disc separation of SW valve SW-82
    .31 (Closed) URI 05000346/2002014-05: Question Regarding Definition of a
      was credible and whether stem-to-disc separation was required to be assumed as part
Passive Failure
      of a passive failure analysis. The team determined that valve SW82 was a butterfly
This URI dealt with the question on whether stem-to-disc separation of SW valve SW-82
      valve. Even if stem-to-disc separation occurred, it was extremely unlikely that flow
was credible and whether stem-to-disc separation was required to be assumed as part
      would be blocked. Therefore, the team determined that this failure mode was not
of a passive failure analysis. The team determined that valve SW82 was a butterfly
      credible and did not need to be considered as part of a passive failure analysis. As
valve. Even if stem-to-disc separation occurred, it was extremely unlikely that flow
      discussed in Sections 4OA3(3)b.11 and 4OA3(3)b.13, the team identified other
would be blocked. Therefore, the team determined that this failure mode was not
      concerns with the licensee's consideration of passive failure assumptions; these
credible and did not need to be considered as part of a passive failure analysis. As
      concerns are addressed separately. This URI is closed.
discussed in Sections 4OA3(3)b.11 and 4OA3(3)b.13, the team identified other
.3     Follow-up on SSDI Findings Documented in Report 05000346/2002019
concerns with the licensee's consideration of passive failure assumptions; these
      (Closed) URI 05000346/2002019-031: Final Evaluation of Apparent Cause
concerns are addressed separately. This URI is closed.
      Evaluation for LER 05000346/2002-006-00
.3
      This URI was opened to track the licensee's resolution of the issues identified in LER
Follow-up on SSDI Findings Documented in Report 05000346/2002019
      05000346/2002-006 on EDG exhaust stack tornado protection. This issue is discussed
   
      in Section 4OA3(3)b.23, of this report. This URI is closed.
(Closed) URI 05000346/2002019-031: Final Evaluation of Apparent Cause
                                                  102                                      Enclosure
Evaluation for LER 05000346/2002-006-00
This URI was opened to track the licensee's resolution of the issues identified in LER
05000346/2002-006 on EDG exhaust stack tornado protection. This issue is discussed
in Section 4OA3(3)b.23, of this report. This URI is closed.


.4   Follow up on Augmented Inspection Team Findings Documented in the Cover
Enclosure
      Letter of Report 05000346/2003016
103
      In the cover letter of IR 05000346/2003016, a number of URIs identified in IR
.4
      05000346/2002008 were converted from URIs to apparent violations (AVs). The
Follow up on Augmented Inspection Team Findings Documented in the Cover
      numbering of the individual items remained the same. The team reviewed the status of
Letter of Report 05000346/2003016
      each of the AVs, as documented below.
In the cover letter of IR 05000346/2003016, a number of URIs identified in IR
  .1 (Discussed) AV 05000346/2003016-01: Technical Specification Reactor Coolant
05000346/2002008 were converted from URIs to apparent violations (AVs). The
      System Pressure Boundary Leakage
numbering of the individual items remained the same. The team reviewed the status of
      Introduction: The NRC team examined corrective actions for an AV of the Davis-Besse
each of the AVs, as documented below.
      TS associated with operation of the plant with pressure boundary leakage from
    .1
      through-wall cracks in the RCS.
(Discussed) AV 05000346/2003016-01: Technical Specification Reactor Coolant
      Description: The team determined that this AV was a product of the licensees cultural
System Pressure Boundary Leakage
      and programmatic breakdowns. Operation with pressure boundary leakage beyond the
Introduction: The NRC team examined corrective actions for an AV of the Davis-Besse
      TS action statement was a direct result of the licensees failure to identify the control rod
TS associated with operation of the plant with pressure boundary leakage from
      drive mechanism leakage. The cultural issues involved the failure to take appropriate
through-wall cracks in the RCS.
      corrective actions, to follow procedures, and to have appropriate procedures; issues that
Description: The team determined that this AV was a product of the licensees cultural
      were identified in the subsequent findings of the AIT follow-up report. The specific
and programmatic breakdowns. Operation with pressure boundary leakage beyond the
      programmatic issues were identified in LER 05000346/2002-002-00 as an inadequate
TS action statement was a direct result of the licensees failure to identify the control rod
      BACC program and inadequate implementation of the ISI program.
drive mechanism leakage. The cultural issues involved the failure to take appropriate
      Corrective actions for the cultural failures were addressed by globally by the licensees
corrective actions, to follow procedures, and to have appropriate procedures; issues that
      management and human performance improvement plan and the program compliance
were identified in the subsequent findings of the AIT follow-up report. The specific
      plan. Corrective actions for the failure to take appropriate action were specified under
programmatic issues were identified in LER 05000346/2002-002-00 as an inadequate
      CR 02-00891 and directed a complete overhaul and re-institution of the CAP. The
BACC program and inadequate implementation of the ISI program.
      NRCs assessment of the effectiveness of those actions is discussed in Sections 4OA2
Corrective actions for the cultural failures were addressed by globally by the licensees
      and 4OA3 of this report.
management and human performance improvement plan and the program compliance
      Corrective action for the inadequate BACC program is discussed below in Section
plan. Corrective actions for the failure to take appropriate action were specified under
      4OA5(1)b.4.8. Inadequate implementation of the ISI program was addressed through
CR 02-00891 and directed a complete overhaul and re-institution of the CAP. The
      licensee self-assessment 2002-081 and a Phase 2 program review by the project review
NRCs assessment of the effectiveness of those actions is discussed in Sections 4OA2
      committee (PRC).
and 4OA3 of this report.
      Analysis: This issue represented a licensee performance deficiency because the
Corrective action for the inadequate BACC program is discussed below in Section
      licensee had multiple opportunities over a period of years to identify the leakage;
4OA5(1)b.4.8. Inadequate implementation of the ISI program was addressed through
      consequently it was considered a finding. This finding was of more than minor safety
licensee self-assessment 2002-081 and a Phase 2 program review by the project review
      significance because the RCPB and resultant cavity in the reactor vessel head
committee (PRC).
      represented a loss of the design basis barrier integrity. Two cornerstones were
Analysis: This issue represented a licensee performance deficiency because the
      impacted by this issue. The barrier integrity cornerstone was affected because the
licensee had multiple opportunities over a period of years to identify the leakage;
      through-wall CRDM cracks compromised the RCPB and the initiating events
consequently it was considered a finding. This finding was of more than minor safety
      cornerstone was impacted because cracking of the CRDM nozzles resulted in an
significance because the RCPB and resultant cavity in the reactor vessel head
      increase in the likelihood of a LOCA.
represented a loss of the design basis barrier integrity. Two cornerstones were
      Enforcement: Davis-Besse TS, "Limiting Condition for Operation for Reactor Coolant
impacted by this issue. The barrier integrity cornerstone was affected because the
      System Operational Leakage," Paragraph 3.4.6.2, stated, in part, that RCS leakage
through-wall CRDM cracks compromised the RCPB and the initiating events
      shall be limited to no pressure boundary leakage, and that with any pressure boundary
cornerstone was impacted because cracking of the CRDM nozzles resulted in an
                                                103                                      Enclosure
increase in the likelihood of a LOCA.
Enforcement: Davis-Besse TS, "Limiting Condition for Operation for Reactor Coolant
System Operational Leakage," Paragraph 3.4.6.2, stated, in part, that RCS leakage
shall be limited to no pressure boundary leakage, and that with any pressure boundary


  leakage, the unit was to be in cold shutdown within 36 hours. This issue was properly
Enclosure
  addressed by the licensees CAP; however, corrective actions were only one of the
104
  inputs into the final characterization and resolution of this item. The NRCs investigation
leakage, the unit was to be in cold shutdown within 36 hours. This issue was properly
  into the cause of this AV, which was referred to the Office of Investigations (OI), is still
addressed by the licensees CAP; however, corrective actions were only one of the
  ongoing. The results of that investigation will be factored into the final enforcement
inputs into the final characterization and resolution of this item. The NRCs investigation
  deliberations. As a result, this item remains open.
into the cause of this AV, which was referred to the Office of Investigations (OI), is still
.2 (Discussed) AV 05000346/2003016-02: Reactor Vessel Head Boric Acid
ongoing. The results of that investigation will be factored into the final enforcement
  Deposits
deliberations. As a result, this item remains open.
  Introduction: The NRC team examined corrective actions for three AVs involving failure
    .2
  to take appropriate corrective actions for continuing or recurrent deficiencies associated
(Discussed) AV 05000346/2003016-02: Reactor Vessel Head Boric Acid
  with boric acid deposits on the reactor vessel head, boric acid deposits on the CACs,
Deposits
  and clogging of radiation element filters.
Introduction: The NRC team examined corrective actions for three AVs involving failure
  Description: The team determined that these AVs were a product of the licensees
to take appropriate corrective actions for continuing or recurrent deficiencies associated
  cultural and programmatic breakdowns. To understand the licensees approach to
with boric acid deposits on the reactor vessel head, boric acid deposits on the CACs,
  correcting these problems, the team examined the licensees root cause analysis report
and clogging of radiation element filters.
  on failure to identify significant degradation of the reactor pressure vessel head. The
Description: The team determined that these AVs were a product of the licensees
  causal factors for these issues were addressed in the root cause report and included:
cultural and programmatic breakdowns. To understand the licensees approach to
  *       Less than adequate safety focus;
correcting these problems, the team examined the licensees root cause analysis report
  *       Less than adequate implementation of the CAP; and
on failure to identify significant degradation of the reactor pressure vessel head. The
  *       No safety analysis performed for the existing condition.
causal factors for these issues were addressed in the root cause report and included:
  Corrective actions for the cultural failure associated with the inadequate safety focus
*
  were addressed by globally by the licensees management and human performance
Less than adequate safety focus;
  improvement plan and the program compliance plan. These were spelled out as
*
  corrective actions to CR 02-00891. Among the corrective actions for these safety
Less than adequate implementation of the CAP; and
  culture issues were:
*
  *       Corrective Action 22: Development of a management field
No safety analysis performed for the existing condition.
          presence/involvement plan to improve management oversight;
Corrective actions for the cultural failure associated with the inadequate safety focus
  *       Corrective Action 41: Formal assessment of the safety conscious work
were addressed by globally by the licensees management and human performance
          environment at the plant based on criteria and attributes derived from NRC policy
improvement plan and the program compliance plan. These were spelled out as
          and guidance;
corrective actions to CR 02-00891. Among the corrective actions for these safety
  *       Corrective Action 42: Changes in corporate and plant senior management;
culture issues were:
  *       Corrective Action 45: Development of a management monitoring process to
*
          monitor and trend the performance of specific management oversight activities;
Corrective Action 22: Development of a management field
  *       Corrective Action 46: Case study training for site personnel to include how the
presence/involvement plan to improve management oversight;
          event happened, what barriers broke down, and what must be different in the
*
          future;
Corrective Action 41: Formal assessment of the safety conscious work
                                            104                                    Enclosure
environment at the plant based on criteria and attributes derived from NRC policy
and guidance;
*
Corrective Action 42: Changes in corporate and plant senior management;
*
Corrective Action 45: Development of a management monitoring process to
monitor and trend the performance of specific management oversight activities;
*
Corrective Action 46: Case study training for site personnel to include how the
event happened, what barriers broke down, and what must be different in the
future;


*       Corrective Action 74: Realignment of management incentives to place more
Enclosure
        reward for safety and safe operation of the station; and
105
*       Corrective Action 75: Establish corporate-wide policy emphasizing the stations
*
        industrial and nuclear safety philosophy.
Corrective Action 74: Realignment of management incentives to place more
reward for safety and safe operation of the station; and
*
Corrective Action 75: Establish corporate-wide policy emphasizing the stations
industrial and nuclear safety philosophy.
Corrective actions for the failure to properly implement the CAP or to perform requisite
Corrective actions for the failure to properly implement the CAP or to perform requisite
safety analyses were specified under CR 02-00891. These directed a complete
safety analyses were specified under CR 02-00891. These directed a complete
overhaul and re-institution of the CAP. To ensure that safety analyses were performed
overhaul and re-institution of the CAP. To ensure that safety analyses were performed
as needed, corporate standards for analyses of safety issues were established and the
as needed, corporate standards for analyses of safety issues were established and the
use of a safety precedence sequence for root cause analyses was mandated. This was
use of a safety precedence sequence for root cause analyses was mandated. This was
confirmed by the team and considered adequate.
confirmed by the team and considered adequate.
The root cause report also identified other, more discrete, issues associated with these
The root cause report also identified other, more discrete, issues associated with these
AVs. These included:
AVs. These included:
*       Addressing symptoms rather than causes;
*
*       Performing less than adequate cause determinations; and
Addressing symptoms rather than causes;
*       Having less than adequate corrective actions.
*
These were also addressed through corrective actions associated with CR 02-00891.
Performing less than adequate cause determinations; and
*
Having less than adequate corrective actions.
These were also addressed through corrective actions associated with CR 02-00891.  
Some of the corrective actions included a case study of this event with an emphasis on
Some of the corrective actions included a case study of this event with an emphasis on
the need to find and address the causes of adverse conditions and the potential
the need to find and address the causes of adverse conditions and the potential
Line 5,093: Line 5,615:
mandating the use of formal root cause techniques coupled with independent reviews
mandating the use of formal root cause techniques coupled with independent reviews
and self-assessments of cause evaluations, and improvements in effectiveness reviews
and self-assessments of cause evaluations, and improvements in effectiveness reviews
with emphasis on verifying that causes have been properly addressed. These were
with emphasis on verifying that causes have been properly addressed. These were
confirmed by the team.
confirmed by the team.
The NRCs assessment of the licensees effectiveness in implementing the revised CAP
The NRCs assessment of the licensees effectiveness in implementing the revised CAP
and the specific actions noted above is discussed in Sections 4OA2 and 4OA3 of this
and the specific actions noted above is discussed in Sections 4OA2 and 4OA3 of this
report.
report.
Analysis: This issue represented a performance deficiency because the licensee failed
Analysis: This issue represented a performance deficiency because the licensee failed
to properly address, either individually or collectively, the cause for the continuing
to properly address, either individually or collectively, the cause for the continuing
accumulation of large amounts of boric acid on the reactor head, the recurrent
accumulation of large amounts of boric acid on the reactor head, the recurrent
deposition of boric acid on CAC fins, and the repeated clogging of radiation element
deposition of boric acid on CAC fins, and the repeated clogging of radiation element
filters. This lack of adequate corrective action on the licensees part contributed to their
filters. This lack of adequate corrective action on the licensees part contributed to their
failure to detect existing through-wall CRDM nozzle cracks and the reactor pressure
failure to detect existing through-wall CRDM nozzle cracks and the reactor pressure
vessel head corrosion. This finding is more than minor because it affected the initiating
vessel head corrosion. This finding is more than minor because it affected the initiating
events cornerstone objective in that cracking of CRDM nozzles represented an increase
events cornerstone objective in that cracking of CRDM nozzles represented an increase
in the likelihood of a LOCA. The barrier integrity cornerstone was also affected in that
in the likelihood of a LOCA. The barrier integrity cornerstone was also affected in that
CRDM cracks resulted in leakage through the RCPB.
CRDM cracks resulted in leakage through the RCPB.
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
conditions adverse to quality be promptly identified and corrected, commensurate with
conditions adverse to quality be promptly identified and corrected, commensurate with
                                        105                                        Enclosure


  their safety significance. Criterion XVI also requires that, for significant conditions
Enclosure
  adverse to quality, the measures assure that the cause of the condition is determined
106
  and that corrective actions were taken to preclude repetition.
their safety significance. Criterion XVI also requires that, for significant conditions
  The team determined that the failure to properly address the continuing accumulation of
adverse to quality, the measures assure that the cause of the condition is determined
  large amounts of boric acid on the reactor head, the recurrent deposition of boric acid
and that corrective actions were taken to preclude repetition.
  on CAC fins, and the repeated clogging of radiation element filters, significant conditions
The team determined that the failure to properly address the continuing accumulation of
  adverse to quality, contributed to the corrosion of the reactor head. These issues have
large amounts of boric acid on the reactor head, the recurrent deposition of boric acid
  been properly addressed by the licensees CAP; however, corrective actions were only
on CAC fins, and the repeated clogging of radiation element filters, significant conditions
  one of the inputs into the final resolution of this item.
adverse to quality, contributed to the corrosion of the reactor head. These issues have
  The NRCs investigation into the cause of this AV, which was referred to OI, is still
been properly addressed by the licensees CAP; however, corrective actions were only
  ongoing. The results of that investigation will be factored into the final enforcement
one of the inputs into the final resolution of this item.
  deliberations. As a result, these items remain open.
The NRCs investigation into the cause of this AV, which was referred to OI, is still
.3 (Discussed) AV 05000346/2003016-03: Containment Air Cooler Boric Acid
ongoing. The results of that investigation will be factored into the final enforcement
  Deposits
deliberations. As a result, these items remain open.
  This issue is included as part of the discussion in Section 4OA5(1)b.4.2 above.
    .3
.4 (Discussed) AV 05000346/2003016-04: Radiation Filter Element Deposits
(Discussed) AV 05000346/2003016-03: Containment Air Cooler Boric Acid
  This issue is included as part of the discussion in Section 4OA5(1)b.4.2 above.
Deposits
.5 (Discussed) AV 05000346/2003016-05: Service Structure Modification Delay
This issue is included as part of the discussion in Section 4OA5(1)b.4.2 above.
  Introduction: The NRC team examined corrective actions for the licensees failure to
    .4
  implement a modification that would have permitted complete inspection and cleaning of
(Discussed) AV 05000346/2003016-04: Radiation Filter Element Deposits
  the reactor vessel head and control rod drive mechanism nozzles.
This issue is included as part of the discussion in Section 4OA5(1)b.4.2 above.
  Description: This issue addressed the licensees repeated deferral of the modification to
    .5
  install multiple access ports in the service structure to permit cleaning and inspection of
(Discussed) AV 05000346/2003016-05: Service Structure Modification Delay
  the reactor head. Modification 90-0012 was initiated in March 1990 to accomplish this
Introduction: The NRC team examined corrective actions for the licensees failure to
  but was deferred twice and then canceled in 1993. The modification was reinitiated in
implement a modification that would have permitted complete inspection and cleaning of
  May 1994 as 94-0025 and subsequently deferred four times before the head
the reactor vessel head and control rod drive mechanism nozzles.
  degradation was identified in 2002.
Description: This issue addressed the licensees repeated deferral of the modification to
  The licensee resolved one portion of the issue through installation of the modification.
install multiple access ports in the service structure to permit cleaning and inspection of
  The repeated deferral was broadly addressed through the management and human
the reactor head. Modification 90-0012 was initiated in March 1990 to accomplish this
  performance improvement plan and the program compliance plan as part of the
but was deferred twice and then canceled in 1993. The modification was reinitiated in
  licensee's itinerary to improve safety culture. The specific issue of deferring
May 1994 as 94-0025 and subsequently deferred four times before the head
  modifications for economic reasons was addressed by corrective actions under
degradation was identified in 2002.
  CR 02-00891 for a revision to the PRC charter. The revision incorporated a requirement
The licensee resolved one portion of the issue through installation of the modification.  
  to include nuclear safety in the considerations when reviewing a plant modification.
The repeated deferral was broadly addressed through the management and human
  Analysis: This issue represented a performance deficiency because the licensee failed
performance improvement plan and the program compliance plan as part of the
  to take corrective action (install the access port modification) for a condition adverse to
licensee's itinerary to improve safety culture. The specific issue of deferring
  quality. As of February 16, 2002, the modification had not been performed, the head
modifications for economic reasons was addressed by corrective actions under
  had not been completely inspected, and the head had not been completely cleaned.
CR 02-00891 for a revision to the PRC charter. The revision incorporated a requirement
                                            106                                      Enclosure
to include nuclear safety in the considerations when reviewing a plant modification.
Analysis: This issue represented a performance deficiency because the licensee failed
to take corrective action (install the access port modification) for a condition adverse to
quality. As of February 16, 2002, the modification had not been performed, the head
had not been completely inspected, and the head had not been completely cleaned.  


  This lack of action on the licensees part, contributed to their failure to detect existing
Enclosure
  through-wall CRDM nozzle cracks.
107
  This finding is more than minor because it affected the initiating events cornerstone
This lack of action on the licensees part, contributed to their failure to detect existing
  objective in that cracking of CRDM nozzles represented an increase in the likelihood of
through-wall CRDM nozzle cracks.
  a LOCA. The barrier integrity cornerstone was also affected in that CRDM cracks
This finding is more than minor because it affected the initiating events cornerstone
  resulted in leakage through the RCPB. Furthermore, the failure to provide for adequate
objective in that cracking of CRDM nozzles represented an increase in the likelihood of
  inspection and cleaning of the head was a contributing factor to the head degradation.
a LOCA. The barrier integrity cornerstone was also affected in that CRDM cracks
  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
resulted in leakage through the RCPB. Furthermore, the failure to provide for adequate
  conditions adverse to quality be promptly identified and corrected. Criterion XVI also
inspection and cleaning of the head was a contributing factor to the head degradation.
  requires that for significant conditions adverse to quality, the measures shall assure that
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that
  the cause of the condition is determined and that corrective actions were taken to
conditions adverse to quality be promptly identified and corrected. Criterion XVI also
  preclude repetition.
requires that for significant conditions adverse to quality, the measures shall assure that
  The licensee failed to correct the condition identified on April 21, 1996 (inability to fully
the cause of the condition is determined and that corrective actions were taken to
  inspect the head and CRDM nozzles), in that, as of February 16, 2002, the corrective
preclude repetition.
  action (modification of the service structure) had not been accomplished. Although
The licensee failed to correct the condition identified on April 21, 1996 (inability to fully
  corrective actions were completed prior to the end of the inspection, corrective actions
inspect the head and CRDM nozzles), in that, as of February 16, 2002, the corrective
  were only one of the inputs into the final characterization and resolution of this item.
action (modification of the service structure) had not been accomplished. Although
  The NRCs investigation into the cause of this AV, which was referred to OI, is still
corrective actions were completed prior to the end of the inspection, corrective actions
  ongoing. The results of that investigation will be factored into the final enforcement
were only one of the inputs into the final characterization and resolution of this item.
  deliberations. As a result, this item remains open.
The NRCs investigation into the cause of this AV, which was referred to OI, is still
.6 (Discussed) AV 05000346/2003016-06: Reactor Coolant System Unidentified
ongoing. The results of that investigation will be factored into the final enforcement
  Leakage Trend
deliberations. As a result, this item remains open.
  Introduction: The NRC team examined corrective actions for a finding involving failure
    .6
  to follow the corrective action procedure and complete a prescribed corrective action for
(Discussed) AV 05000346/2003016-06: Reactor Coolant System Unidentified
  adverse trends in RCS unidentified leakage.
Leakage Trend
  Description: This URI addressed the licensees cancellation of a Mode 3 walkdown that
Introduction: The NRC team examined corrective actions for a finding involving failure
  was the proposed corrective action for an adverse trend in RCS unidentified leakage.
to follow the corrective action procedure and complete a prescribed corrective action for
  Several months prior to the shutdown for the 2002 refueling outage the licensee had
adverse trends in RCS unidentified leakage.
  been examining increases in RCS leakage and as part of an extensive investigation, a
Description: This URI addressed the licensees cancellation of a Mode 3 walkdown that
  walkdown of the containment while the plant was at NOP/NOT had been specified. The
was the proposed corrective action for an adverse trend in RCS unidentified leakage.  
  reason for canceling the walkdown was schedule-driven; a special Mode 3 walkdown
Several months prior to the shutdown for the 2002 refueling outage the licensee had
  would have delayed cooldown and entry into the lower modes required to begin
been examining increases in RCS leakage and as part of an extensive investigation, a
  refueling.
walkdown of the containment while the plant was at NOP/NOT had been specified. The
  The team concluded that the root cause for this was the licensees cultural and
reason for canceling the walkdown was schedule-driven; a special Mode 3 walkdown
  programmatic breakdowns. The licensees root cause analysis report pointed to the
would have delayed cooldown and entry into the lower modes required to begin
  following causal factors:
refueling.
  *       Less than adequate safety focus;
The team concluded that the root cause for this was the licensees cultural and
  *       Less than adequate implementation of the CAP; and
programmatic breakdowns. The licensees root cause analysis report pointed to the
  *       Less than adequate corrective actions.
following causal factors:
                                            107                                        Enclosure
*
Less than adequate safety focus;
*
Less than adequate implementation of the CAP; and
*
Less than adequate corrective actions.


  Corrective actions for the cultural failure associated with the inadequate safety focus
Enclosure
  were addressed globally by the licensees management and human performance
108
  improvement plan and the program compliance plan and are discussed in Section
Corrective actions for the cultural failure associated with the inadequate safety focus
  4OA5(1)b.4.2 above. Corrective actions for the failure to properly implement the CAP
were addressed globally by the licensees management and human performance
  were specified under CR 02-00891. These directed a complete overhaul and
improvement plan and the program compliance plan and are discussed in Section
  re-institution of the CAP. The NRCs assessment of the licensees effectiveness in
4OA5(1)b.4.2 above. Corrective actions for the failure to properly implement the CAP
  implementing the revised CAP and the specific actions noted above is discussed in
were specified under CR 02-00891. These directed a complete overhaul and
  Sections 4OA2 and 4OA3 of this report.
re-institution of the CAP. The NRCs assessment of the licensees effectiveness in
  Analysis: This issue represented a the licensee performance deficiency because
implementing the revised CAP and the specific actions noted above is discussed in
  elimination of a key component of what was an adequate proposed corrective action
Sections 4OA2 and 4OA3 of this report.
  rendered the proposal inadequate. Consequently, this was considered a finding
Analysis: This issue represented a the licensee performance deficiency because
  because it was reflective of other corrective action deficiencies which contributed to the
elimination of a key component of what was an adequate proposed corrective action
  cavity in the reactor vessel head. This finding was of more than minor safety
rendered the proposal inadequate. Consequently, this was considered a finding
  significance because the corrosion of the reactor head and the resulting cavity
because it was reflective of other corrective action deficiencies which contributed to the
  represented a significant loss of the design basis barrier integrity.
cavity in the reactor vessel head. This finding was of more than minor safety
  Enforcement: The licensee failed to follow the corrective action procedure and
significance because the corrosion of the reactor head and the resulting cavity
  implement an effective corrective action for adverse trends in RCS unidentified leakage.
represented a significant loss of the design basis barrier integrity.
  Although corrective actions have now been completed, corrective actions were only one
Enforcement: The licensee failed to follow the corrective action procedure and
  of the inputs into the final characterization and resolution of this item.
implement an effective corrective action for adverse trends in RCS unidentified leakage.  
  The NRCs investigation into the cause of this finding, which was referred to OI, is still
Although corrective actions have now been completed, corrective actions were only one
  ongoing. The results of that investigation will be factored into the final enforcement
of the inputs into the final characterization and resolution of this item.
  deliberations. As a result, this item remains open.
The NRCs investigation into the cause of this finding, which was referred to OI, is still
.7 (Discussed) AV 05000346/2003016-07: Inadequate Boric Acid Corrosion
ongoing. The results of that investigation will be factored into the final enforcement
  Control Program Procedure
deliberations. As a result, this item remains open.
  Introduction: The NRC team examined corrective actions for the licensees failure to
    .7
  have a BACC program procedure appropriate to the circumstances.
(Discussed) AV 05000346/2003016-07: Inadequate Boric Acid Corrosion
  Description: The AIT follow-up inspection and the licensees root cause report identified
Control Program Procedure
  multiple deficiencies in the licensee's BACC program procedure which contributed to the
Introduction: The NRC team examined corrective actions for the licensees failure to
  degradation of the reactor head. As part of the licensees program compliance plan, the
have a BACC program procedure appropriate to the circumstances.
  BACC program procedure was completely revised and subjected to a phase 2 PRB
Description: The AIT follow-up inspection and the licensees root cause report identified
  review. The program compliance plan, the PRC review, and the revised BACC program
multiple deficiencies in the licensee's BACC program procedure which contributed to the
  procedure were inspected and accepted by NRC; this inspection was documented in IR
degradation of the reactor head. As part of the licensees program compliance plan, the
  05000346-03-09;05000346-03-11.
BACC program procedure was completely revised and subjected to a phase 2 PRB
  Analysis: This issue represented a the licensee performance deficiency because the
review. The program compliance plan, the PRC review, and the revised BACC program
  weaknesses in the procedure contributed to the failure, over a period of years, by the
procedure were inspected and accepted by NRC; this inspection was documented in IR
  licensees engineering staff to properly identify and evaluate the leaking CRDM nozzle
05000346-03-09;05000346-03-11.
  and the expanding cavity in the reactor head. This finding is more than minor because it
Analysis: This issue represented a the licensee performance deficiency because the
  affected the initiating events cornerstone objective in that cracking of CRDM nozzles
weaknesses in the procedure contributed to the failure, over a period of years, by the
  represented an increase in the likelihood of a LOCA. The barrier integrity cornerstone
licensees engineering staff to properly identify and evaluate the leaking CRDM nozzle
  was also affected in that CRDM cracks resulted in leakage through the RCPB.
and the expanding cavity in the reactor head. This finding is more than minor because it
                                            108                                    Enclosure
affected the initiating events cornerstone objective in that cracking of CRDM nozzles
represented an increase in the likelihood of a LOCA. The barrier integrity cornerstone
was also affected in that CRDM cracks resulted in leakage through the RCPB.


  Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, states, in part, that
Enclosure
  activities affecting quality shall be prescribed by documented instructions, procedures,
109
  or drawings, of a type appropriate to the circumstances and shall be accomplished in
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, states, in part, that
  accordance with these instructions, procedures, or drawings.
activities affecting quality shall be prescribed by documented instructions, procedures,
  NG-EN-00324, "Boric Acid Corrosion Control Program," Revisions 0 through 2, were
or drawings, of a type appropriate to the circumstances and shall be accomplished in
  classified as a quality procedure under the licensees procedure administrative system
accordance with these instructions, procedures, or drawings.
  and were not appropriate to the circumstances in that deficiencies in the procedure
NG-EN-00324, "Boric Acid Corrosion Control Program," Revisions 0 through 2, were
  contributed to the failure to detect and address corrosion of the reactor head. Although
classified as a quality procedure under the licensees procedure administrative system
  corrective actions have now been completed, corrective actions were only one of the
and were not appropriate to the circumstances in that deficiencies in the procedure
  inputs into the final characterization and resolution of this item.
contributed to the failure to detect and address corrosion of the reactor head. Although
  The NRCs investigation into the cause of this AV, which was referred to OI, is still
corrective actions have now been completed, corrective actions were only one of the
  ongoing. The results of that investigation will be factored into the final enforcement
inputs into the final characterization and resolution of this item.
  deliberations. As a result, this item remains open.
The NRCs investigation into the cause of this AV, which was referred to OI, is still
.8 (Discussed) AV 05000346/2003016-08: Failure to Follow Boric Acid Corrosion
ongoing. The results of that investigation will be factored into the final enforcement
  Control Program Procedure
deliberations. As a result, this item remains open.
  Introduction: The NRC team examined corrective actions for two AVs involving failure to
    .8
  follow the boric acid corrosion control program procedure and the corrective actions
(Discussed) AV 05000346/2003016-08: Failure to Follow Boric Acid Corrosion
  program procedure.
Control Program Procedure
  Description: These URIs involved failure by the licensee engineering staff to follow:
Introduction: The NRC team examined corrective actions for two AVs involving failure to
  *       A number of requirements of the BACC program procedure, most notably the
follow the boric acid corrosion control program procedure and the corrective actions
            requirement to remove all boric acid and examine the base metal underneath for
program procedure.
            signs of corrosion; and
Description: These URIs involved failure by the licensee engineering staff to follow:
  *       The guidance and examples for characterization of CRs as significant, important,
*
            routine, or non-conditions adverse to quality and, as a result, repeatedly
A number of requirements of the BACC program procedure, most notably the
            mis-characterized the conditions on the reactor head as routine.
requirement to remove all boric acid and examine the base metal underneath for
  The team reviewed the sections of the licensees root cause report which acknowledged
signs of corrosion; and
  these two issues, the section of the root cause report which outlined corrective actions,
*
  and the corrective action specified under CR 02-00891. To correct the failure to follow
The guidance and examples for characterization of CRs as significant, important,
  the boric acid corrosion control program procedure, the licensee developed these
routine, or non-conditions adverse to quality and, as a result, repeatedly
  specific actions:
mis-characterized the conditions on the reactor head as routine.
  *       Provide training to applicable personnel and mangers on the need to remove
The team reviewed the sections of the licensees root cause report which acknowledged
            boric acid from components, to inspect for signs of corrosion, and to perform
these two issues, the section of the root cause report which outlined corrective actions,
            inspections for signs of boric acid in component internals; and
and the corrective action specified under CR 02-00891. To correct the failure to follow
  *       Reinforce standards and expectations for procedure compliance and the need
the boric acid corrosion control program procedure, the licensee developed these
            for work practice rigor.
specific actions:
  These were part of the licensees global approach to the safety culture issue as part of
*
  the management and human performance improvement plan and the program
Provide training to applicable personnel and mangers on the need to remove
  compliance plan.
boric acid from components, to inspect for signs of corrosion, and to perform
                                            109                                    Enclosure
inspections for signs of boric acid in component internals; and
*
Reinforce standards and expectations for procedure compliance and the need
for work practice rigor.
These were part of the licensees global approach to the safety culture issue as part of
the management and human performance improvement plan and the program
compliance plan.


      In the root cause, the licensee acknowledged that CRs associated with the reactor head
Enclosure
      and other boric acid conditions were categorized as relatively low, which resulted in the
110
      use of superficial cause analysis techniques. To address this, the licensee developed
In the root cause, the licensee acknowledged that CRs associated with the reactor head
      two corrective actions:
and other boric acid conditions were categorized as relatively low, which resulted in the
      *       Establish and ensure that criteria for categorization of the significance of repeat
use of superficial cause analysis techniques. To address this, the licensee developed
              equipment failures were appropriate and used by station personnel. Criteria
two corrective actions:
              were to be sufficient to elevate repeat problems to higher levels, which require
*
              use of more robust analyses; and
Establish and ensure that criteria for categorization of the significance of repeat
      *       Review existing long-standing issues for possible elevation to significant
equipment failures were appropriate and used by station personnel. Criteria
              condition status, thus engaging formal root cause evaluation techniques to
were to be sufficient to elevate repeat problems to higher levels, which require
              obtain resolution of the issues.
use of more robust analyses; and
      As part of the program compliance inspection and the corrective actions team
*
      inspection, both of these actions were verified to have been satisfactorily completed.
Review existing long-standing issues for possible elevation to significant
      Analysis: This issue represented a performance deficiency because the recurrent
condition status, thus engaging formal root cause evaluation techniques to
      failures, by the licensees engineering staff, to follow the BACC program and CAP
obtain resolution of the issues.
      procedures resulted in the perpetuation of the CRDM nozzle leak and the development
As part of the program compliance inspection and the corrective actions team
      of the expanding cavity in the reactor head. This finding was of more than minor safety
inspection, both of these actions were verified to have been satisfactorily completed.
      significance because the cavity in the reactor vessel head represented a loss of the
Analysis: This issue represented a performance deficiency because the recurrent
      design basis barrier integrity.
failures, by the licensees engineering staff, to follow the BACC program and CAP
      Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V states, in part, that
procedures resulted in the perpetuation of the CRDM nozzle leak and the development
      activities affecting quality shall be prescribed by documented instructions, procedures,
of the expanding cavity in the reactor head. This finding was of more than minor safety
      or drawings, of a type appropriate to the circumstances and shall be accomplished in
significance because the cavity in the reactor vessel head represented a loss of the
      accordance with these instructions, procedures, or drawings.
design basis barrier integrity.
      The licensees engineering staff failed, on multiple occasions, to adhere to both the
Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V states, in part, that
      BACC program and the CAP procedures. Although corrective actions have now been
activities affecting quality shall be prescribed by documented instructions, procedures,
      completed, corrective actions were only one of the inputs into the final characterization
or drawings, of a type appropriate to the circumstances and shall be accomplished in
      and resolution of this item.
accordance with these instructions, procedures, or drawings.
      The NRCs investigation into the cause of this AV, which was referred to OI, is still
The licensees engineering staff failed, on multiple occasions, to adhere to both the
      ongoing. The results of that investigation will be factored into the final enforcement
BACC program and the CAP procedures. Although corrective actions have now been
      deliberations. As a result, this item remains open.
completed, corrective actions were only one of the inputs into the final characterization
  .9 (Discussed) AV 05000346/2003016-09: Failure to Follow Corrective Action
and resolution of this item.
      Program Procedure
The NRCs investigation into the cause of this AV, which was referred to OI, is still
      This item is included as part of the discussion in Section 4OA5(1)b.4.8 above.
ongoing. The results of that investigation will be factored into the final enforcement
(2)   Closure of Restart Checklist Items
deliberations. As a result, this item remains open.
  .1 Restart Checklist Item 2.c: Structures, Systems, and Components Inside
    .9
      Containment
(Discussed) AV 05000346/2003016-09: Failure to Follow Corrective Action
      As part of the corrective actions resulting from the reactor vessel head degradation, the
Program Procedure
      licensee established a return to service plan to identify, monitor, and control all actions
This item is included as part of the discussion in Section 4OA5(1)b.4.8 above.
                                                110                                      Enclosure
(2)
Closure of Restart Checklist Items
    .1
Restart Checklist Item 2.c: Structures, Systems, and Components Inside
Containment
As part of the corrective actions resulting from the reactor vessel head degradation, the
licensee established a return to service plan to identify, monitor, and control all actions


  necessary for the safe and reliable return to service of Davis-Besse. The plan consisted
Enclosure
  of seven building blocks designed to support safe and reliable restart of the plant and to
111
  ensure sustained performance improvements. One of the building blocks, "Containment
necessary for the safe and reliable return to service of Davis-Besse. The plan consisted
  Extent of Condition Program," was tasked with evaluating and dispositioning the extent
of seven building blocks designed to support safe and reliable restart of the plant and to
  of condition throughout the RCS and containment systems, structures, and components
ensure sustained performance improvements. One of the building blocks, "Containment
  relative to the degradation mechanisms that occurred on the reactor vessel head.
Extent of Condition Program," was tasked with evaluating and dispositioning the extent
  IR 05000346/2002009 reviewed the licensees plan for inspections, including methods,
of condition throughout the RCS and containment systems, structures, and components
  control of walkdown boundaries, resolution of obstructed examinations, and control of
relative to the degradation mechanisms that occurred on the reactor vessel head.
  inspection records. Two findings of very low safety significance were identified. The
IR 05000346/2002009 reviewed the licensees plan for inspections, including methods,
  first was associated with lack of acceptance criteria and the second was associated with
control of walkdown boundaries, resolution of obstructed examinations, and control of
  inadequate training and certification of inspection personnel. Weaknesses were
inspection records. Two findings of very low safety significance were identified. The
  identified in the licensees implementation of the containment inspection program.
first was associated with lack of acceptance criteria and the second was associated with
  IR 05000346/2002012 focused on evaluating corrective actions for the issues previously
inadequate training and certification of inspection personnel. Weaknesses were
  identified. This inspection concluded that the above issues were adequately resolved
identified in the licensees implementation of the containment inspection program.
  and that the inspections were effectively implemented. Three URIs associated with
IR 05000346/2002012 focused on evaluating corrective actions for the issues previously
  corrective actions for corrosion of electrical conduit, potential leakage of reactor vessel
identified. This inspection concluded that the above issues were adequately resolved
  bottom head incore instrumentation penetrations, and failure to follow the procedure for
and that the inspections were effectively implemented. Three URIs associated with
  Raychem' splice removal on electrical cable were identified. Restart Checklist Item 2.c
corrective actions for corrosion of electrical conduit, potential leakage of reactor vessel
  was held open pending review of these URIs.
bottom head incore instrumentation penetrations, and failure to follow the procedure for
  Unresolved item 05000346/2002012-01 was discussed and closed in IR
Raychem' splice removal on electrical cable were identified. Restart Checklist Item 2.c
  05000346-03-23. The NRC reviewed the licensees activities to resolve the potential
was held open pending review of these URIs.
  leakage of reactor vessel bottom head incore instrumentation penetrations. The
Unresolved item 05000346/2002012-01 was discussed and closed in IR
  licensee performed chemical analysis of the deposits found on the reactor vessel sides
05000346-03-23. The NRC reviewed the licensees activities to resolve the potential
  and bottom, and in a July 30, 2003, letter to the NRC, concluded that the deposits did
leakage of reactor vessel bottom head incore instrumentation penetrations. The
  not result from leakage from the penetrations. Additionally, the bottom head was
licensee performed chemical analysis of the deposits found on the reactor vessel sides
  inspected for signs of leakage after completion of the seven day NOP/NOT leak test.
and bottom, and in a July 30, 2003, letter to the NRC, concluded that the deposits did
  This test provided reasonable assurance that the bottom head penetrations were not
not result from leakage from the penetrations. Additionally, the bottom head was
  leaking.
inspected for signs of leakage after completion of the seven day NOP/NOT leak test.  
  Unresolved item 05000346/2002012-02 concerning corrosion of electrical conduit is
This test provided reasonable assurance that the bottom head penetrations were not
  discussed and closed in Section 4OA5(1)b.1.1 of this report.
leaking.
  Unresolved item 05000346/2002012-03 concerning removal of Raychem' splices from
Unresolved item 05000346/2002012-02 concerning corrosion of electrical conduit is
  electrical cable is discussed in Section 4OA3(2)b.6 and the URI is closed in Section
discussed and closed in Section 4OA5(1)b.1.1 of this report.
  4OA5(1)b.1.2.
Unresolved item 05000346/2002012-03 concerning removal of Raychem' splices from
  On November 18, 2003, the Davis-Besse Oversight Panel met to discuss this issue and
electrical cable is discussed in Section 4OA3(2)b.6 and the URI is closed in Section
  concluded that Restart Checklist Item 2.c is closed.
4OA5(1)b.1.2.
.2 Restart Checklist Item 3.a: Corrective Action Program
On November 18, 2003, the Davis-Besse Oversight Panel met to discuss this issue and
  As part of the corrective actions resulting from the reactor vessel head degradation, the
concluded that Restart Checklist Item 2.c is closed.
  licensee established a return to service plan to identify, monitor, and control all actions
    .2
  necessary for the safe and reliable return to service of Davis-Besse. A key element of
Restart Checklist Item 3.a: Corrective Action Program
  the return to service plan was for the licensee to reestablish and reinvigorate the CAP to
As part of the corrective actions resulting from the reactor vessel head degradation, the
  ensure that future conditions adverse to quality were properly identified, evaluated and
licensee established a return to service plan to identify, monitor, and control all actions
                                            111                                      Enclosure
necessary for the safe and reliable return to service of Davis-Besse. A key element of
the return to service plan was for the licensee to reestablish and reinvigorate the CAP to
ensure that future conditions adverse to quality were properly identified, evaluated and


  corrected. The NRC performed a review of the CAP which was documented in NRC
Enclosure
  Inspection Report Nos. 50-346/02-11 and 50-346/03-09 and found the program to be
112
  acceptable. Restart Checklist item 3.a was left open following these inspections,
corrected. The NRC performed a review of the CAP which was documented in NRC
  pending completion of the CATI.
Inspection Report Nos. 50-346/02-11 and 50-346/03-09 and found the program to be
  The main function of the CATI inspection, described in the report above, was to evaluate
acceptable. Restart Checklist item 3.a was left open following these inspections,
  the licensees effectiveness in correcting the deficiencies in the CAP. As noted in the
pending completion of the CATI.
  previous sections of the report, the team identified numerous deficiencies still existing
The main function of the CATI inspection, described in the report above, was to evaluate
  within the CAP. Nevertheless, the team concluded that the licensees corrective actions
the licensees effectiveness in correcting the deficiencies in the CAP. As noted in the
  were acceptable to support plant restart.
previous sections of the report, the team identified numerous deficiencies still existing
  These deficiencies were discussed with the licensee during two public meetings, one on
within the CAP. Nevertheless, the team concluded that the licensees corrective actions
  November 12, and a second on December 10, 2003. As part of these meetings, the
were acceptable to support plant restart.
  licensee made a number of commitments to further improve the CAP as part of its
These deficiencies were discussed with the licensee during two public meetings, one on
  Operational Improvement Plan for Cycle 14, Revision 2.
November 12, and a second on December 10, 2003. As part of these meetings, the
  The team presented the results of this inspection to the NRC Davis-Besse Oversight
licensee made a number of commitments to further improve the CAP as part of its
  Panel on February 5, 2004. The panel concluded that, based upon the licensees
Operational Improvement Plan for Cycle 14, Revision 2.
  improvement plans, Restart Checklist Item 3.a could be closed.
The team presented the results of this inspection to the NRC Davis-Besse Oversight
.3 Restart Checklist Item 5.b: Systems Readiness for Restart
Panel on February 5, 2004. The panel concluded that, based upon the licensees
  As part of the corrective actions resulting from the reactor vessel head degradation, the
improvement plans, Restart Checklist Item 3.a could be closed.
  licensee established a return to service plan to identify, monitor, and control all actions
    .3
  necessary for the safe and reliable return to service of Davis-Besse. One of the key
Restart Checklist Item 5.b: Systems Readiness for Restart
  elements of this return to service plan was a systematic review of a number of
As part of the corrective actions resulting from the reactor vessel head degradation, the
  safety-related systems.
licensee established a return to service plan to identify, monitor, and control all actions
  Concurrent with the licensees initial evaluation of the systems, the NRC performed a
necessary for the safe and reliable return to service of Davis-Besse. One of the key
  SSDI as documented in IR 05000346/2002014. This inspection identified a large
elements of this return to service plan was a systematic review of a number of
  number of NCVs and URIs which required resolution to ensure system operability prior
safety-related systems.
  to restart. As part of this inspection effort, the team evaluated the adequacy of the
Concurrent with the licensees initial evaluation of the systems, the NRC performed a
  licensees corrective actions to address and resolve the identified deficiencies.
SSDI as documented in IR 05000346/2002014. This inspection identified a large
  The teams findings and conclusions documented in this report revealed weaknesses in
number of NCVs and URIs which required resolution to ensure system operability prior
  the licensees implementation of corrective actions and in the engineering rigor to
to restart. As part of this inspection effort, the team evaluated the adequacy of the
  address and resolve identified deficiencies. Throughout the inspection, the team also
licensees corrective actions to address and resolve the identified deficiencies.
  made observations and reached conclusions regarding the safety significance of the
The teams findings and conclusions documented in this report revealed weaknesses in
  identified deficiencies and ability of affected components to perform the intended design
the licensees implementation of corrective actions and in the engineering rigor to
  function. Concerns and issues were presented to the licensee for entry into their
address and resolve identified deficiencies. Throughout the inspection, the team also
  corrective action program and final implementation of corrective actions. The teams
made observations and reached conclusions regarding the safety significance of the
  inspection did not reach a conclusion regarding the readiness of systems to support
identified deficiencies and ability of affected components to perform the intended design
  restart since during the teams inspection, the licensee was still in the process of
function. Concerns and issues were presented to the licensee for entry into their
  returning systems to functional and operational status. Therefore, restart checklist item
corrective action program and final implementation of corrective actions. The teams
  5.b remains open, and will be further addressed in a separate NRC inspection report.
inspection did not reach a conclusion regarding the readiness of systems to support
                                            112                                      Enclosure
restart since during the teams inspection, the licensee was still in the process of
returning systems to functional and operational status. Therefore, restart checklist item
5.b remains open, and will be further addressed in a separate NRC inspection report.


Enclosure
113
4OA6 Management Meetings
4OA6 Management Meetings
    Exit Meeting Summary
Exit Meeting Summary
    The team presented the inspection results to Mr. L. Myers and other members of
The team presented the inspection results to Mr. L. Myers and other members of
    licensee management and staff at the conclusion of the inspection on September 9,
licensee management and staff at the conclusion of the inspection on September 9,
    2003. The licensee acknowledged the information presented.
2003. The licensee acknowledged the information presented.
    Per the licensees request, on November 10, 2003, the team presented the latest
Per the licensees request, on November 10, 2003, the team presented the latest
    inspection results, during a telephone conference, to Mr. L. Myers and other members of
inspection results, during a telephone conference, to Mr. L. Myers and other members of
    the licensee management and staff. The licensee acknowledged the information
the licensee management and staff. The licensee acknowledged the information
    presented.
presented.
    On January 7, 2004, the team held a telephone exit with the licensee in regard to the
On January 7, 2004, the team held a telephone exit with the licensee in regard to the
    HPI minimum flow issue discussed in Section 4OA3(3)b.1.
HPI minimum flow issue discussed in Section 4OA3(3)b.1.
ATTACHMENT: SUPPLEMENTAL INFORMATION
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                            113                                    Enclosure


                                SUPPLEMENTAL INFORMATION
Attachment
                                  KEY POINTS OF CONTACT
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
Licensee
M. Bezilla, Site Vice President
M. Bezilla, Site Vice President
Line 5,427: Line 5,977:
W. Marini, Regulatory Interface
W. Marini, Regulatory Interface
M. Marler, Training Manager
M. Marler, Training Manager
L. Myers, Chief Operating Officer, FENOC
L. Myers, Chief Operating Officer, FENOC  
K. Ostrawski, Manager, Regulatory Affairs
K. Ostrawski, Manager, Regulatory Affairs
W. Pearce, Vice President, Oversight
W. Pearce, Vice President, Oversight
Line 5,444: Line 5,994:
J. Rutkowski, Resident Inspector
J. Rutkowski, Resident Inspector
S. Thomas, Senior Resident Inspector
S. Thomas, Senior Resident Inspector
                                                                                Attachment


                  LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Attachment
A2
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
Opened
05000346/2003010-01       VIO Failure to Take Corrective Actions for a Previous NCV
05000346/2003010-01
                                Concerning SW Discharge Path Swapover Setpoints
VIO
                                (Section 4OA3(3)b.11)
Failure to Take Corrective Actions for a Previous NCV
05000346/2003010-02       VIO Failure to Take Corrective Actions for a Previous NCV
Concerning SW Discharge Path Swapover Setpoints  
                                Concerning SW Pump Discharge Check Valve
(Section 4OA3(3)b.11)
                                Acceptance Criteria (Section 4OA3(3)b.12)
05000346/2003010-02
VIO
Failure to Take Corrective Actions for a Previous NCV
Concerning SW Pump Discharge Check Valve
Acceptance Criteria (Section 4OA3(3)b.12)
Open and Closed in This Report
Open and Closed in This Report
05000346/2003010-03       NCV Undervoltage Time Delay Relay Setting Did Not Account
05000346/2003010-03
                                For Instrument Uncertainties (Section 4OA3(2)b.1)
NCV
05000346/2003010-04       NCV Lack of 480 Vac Class 1E Motor Thermal Overload
Undervoltage Time Delay Relay Setting Did Not Account
                                Protection (Section 4OA3(2)b.2)
For Instrument Uncertainties (Section 4OA3(2)b.1)
05000346/2003010-05       NCV Failure to Perform Adequate Direct Current Contactor
05000346/2003010-04
                                Testing to Ensure Minimum Voltage at Motor Operated
NCV
                                Valves (Section 4OA3(2)b.3)
Lack of 480 Vac Class 1E Motor Thermal Overload
05000346/2003010-06       NCV Failure to Verify Adequacy of Short Circuit Protection for
Protection (Section 4OA3(2)b.2)
                                Direct Current Circuits (Section 4OA3(2)b.4)
05000346/2003010-05
05000346/2003010-07       NCV Lack of Calculations to Ensure Minimum Voltage
NCV
                                Availability at Device Terminals (Section 4OA3(2)b.5)
Failure to Perform Adequate Direct Current Contactor
05000346/2003010-08       NCV Failure to Verify Adequacy of HPI Minimum Recirculation
Testing to Ensure Minimum Voltage at Motor Operated
                                Line Design (Section 4OA3(3)b.1)
Valves (Section 4OA3(2)b.3)
05000346/2003010-09       NCV Increased Dose Consequences Due to Degraded Thermal
05000346/2003010-06
                                Performance Operation of Degraded CAC (Section
NCV
                                4OA3(3)b.2)
Failure to Verify Adequacy of Short Circuit Protection for
05000346/2003010-10       NCV Containment Air Cooler Air Flow Calculation Concerns
Direct Current Circuits (Section 4OA3(2)b.4)
                                (Section 4OA3(3)b.3)
05000346/2003010-07
05000346/2003010-11       NCV Accumulator Sizing Calculation Errors (Section
NCV
                                4OA3(3)b.4)
Lack of Calculations to Ensure Minimum Voltage
05000346/2003010-12       NCV Non-conservative Calculation Used in Design Analysis to
Availability at Device Terminals (Section 4OA3(2)b.5)
                                Determine Required Service Water Makeup Flow to
05000346/2003010-08
                                Component Cooling Water (Section 4OA3(3)b.6)
NCV
05000346/2003010-13       NCV Calculation Concerns for Service Water Pump Room
Failure to Verify Adequacy of HPI Minimum Recirculation
                                Ventilation System (Section 4OA3(3)b.7)
Line Design (Section 4OA3(3)b.1)
                                          A2                                  Attachment
05000346/2003010-09
NCV
Increased Dose Consequences Due to Degraded Thermal
Performance Operation of Degraded CAC (Section
4OA3(3)b.2)
05000346/2003010-10
NCV
Containment Air Cooler Air Flow Calculation Concerns  
(Section 4OA3(3)b.3)
05000346/2003010-11
NCV
Accumulator Sizing Calculation Errors (Section
4OA3(3)b.4)
05000346/2003010-12
NCV
Non-conservative Calculation Used in Design Analysis to
Determine Required Service Water Makeup Flow to
Component Cooling Water (Section 4OA3(3)b.6)
05000346/2003010-13
NCV
Calculation Concerns for Service Water Pump Room
Ventilation System (Section 4OA3(3)b.7)


              LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
05000346/2003010-14     NCV Inadequate Service Water System Flow Analysis (Section
Attachment
                              4OA3(3)b.8)
A3
05000346/2003010-15     NCV Inadequate Flooding Protection for the Service Water
05000346/2003010-14
                              System (Section 4OA3(3)b.9)
NCV
05000346/2003010-16     NCV Inadequate Service Water System Flow Balance Testing
Inadequate Service Water System Flow Analysis (Section
                              Procedure (Section 4OA3(3)b.10)
4OA3(3)b.8)
05000346/2003010-17     NCV Lack of Design Basis Calculations to Support Service
05000346/2003010-15
                              Water Valve Single Failure Assumptions (Section
NCV
                              4OA3(3)b.13)
Inadequate Flooding Protection for the Service Water
05000346/2003010-18     NCV Auxiliary Feedwater System Calculation Issues With Main
System (Section 4OA3(3)b.9)
                              Steam Safety Valves (Section 4OA3(3)b.14)
05000346/2003010-16
05000346/2003010-19     NCV Preconditioning of Auxiliary Feedwater System During
NCV
                              Testing (Section 4OA3(3)b.15)
Inadequate Service Water System Flow Balance Testing
05000346/2003010-20     NCV Borated Water Storage Tank Calculation Issues (Section
Procedure (Section 4OA3(3)b.10)
                              4OA3(3)b.18)
05000346/2003010-17
05000346/2003010-21     NCV Inadequate Evaluation of Reactor Coolant Pump
NCV
                              Casing-to-cover Stud Overstressing (Section
Lack of Design Basis Calculations to Support Service
                              4OA3(3)b.19)
Water Valve Single Failure Assumptions (Section
05000346/2003010-22     NCV ECCS Motors Not Qualified for Service Time (Section
4OA3(3)b.13)
                              4OA3(3)b.21)
05000346/2003010-18
05000346/2003010-23     NCV Inappropriate Application of 10 CFR 50.59 (Section
NCV
                              4OA3(3)b.23)
Auxiliary Feedwater System Calculation Issues With Main
05000346/2003010-24     NCV Failure to Perform Comprehensive Moderate Energy Line
Steam Safety Valves (Section 4OA3(3)b.14)
                              Break Analysis (Section 4OA3(3)b.24)
05000346/2003010-19
05000346/2003010-25     NCV Repetitive Spacer Grid Strap Damage (Section 4OA3(4)b)
NCV
05000346/2003010-26     NCV Process Monitoring Function for Alternative Shutdown
Preconditioning of Auxiliary Feedwater System During
                              Capability (Section 4OA3(5)b.1)
Testing (Section 4OA3(3)b.15)
05000346/2003010-27     NCV Supporting Functions for Alternative Shutdown Capability
05000346/2003010-20
                              (Section 4OA3(5)b.2)
NCV
05000346/2003010-28     NCV Emergency Diesel Generator Floor Drains Design
Borated Water Storage Tank Calculation Issues (Section
                              Deficiency (Section 4OA3(5)b.3)
4OA3(3)b.18)
                                        A3                                  Attachment
05000346/2003010-21
NCV
Inadequate Evaluation of Reactor Coolant Pump
Casing-to-cover Stud Overstressing (Section
4OA3(3)b.19)
05000346/2003010-22
NCV
ECCS Motors Not Qualified for Service Time (Section
4OA3(3)b.21)
05000346/2003010-23
NCV
Inappropriate Application of 10 CFR 50.59 (Section
4OA3(3)b.23)
05000346/2003010-24
NCV
Failure to Perform Comprehensive Moderate Energy Line
Break Analysis (Section 4OA3(3)b.24)
05000346/2003010-25
NCV
Repetitive Spacer Grid Strap Damage (Section 4OA3(4)b)
05000346/2003010-26
NCV
Process Monitoring Function for Alternative Shutdown
Capability (Section 4OA3(5)b.1)
05000346/2003010-27
NCV
Supporting Functions for Alternative Shutdown Capability  
(Section 4OA3(5)b.2)
05000346/2003010-28
NCV
Emergency Diesel Generator Floor Drains Design
Deficiency (Section 4OA3(5)b.3)


              LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
05000346/2003010-29     NCV Failure to Provide HPI Recirculation Line (Section
Attachment
                              4OA3(6)b.3)
A4
05000346/2003010-29
NCV
Failure to Provide HPI Recirculation Line (Section
4OA3(6)b.3)
Closed
Closed
05000346/2002-009-00     LER Degradation of the High Pressure Injection Thermal
05000346/2002-009-00
                              Sleeves
LER
05000346/2002012-02     URI Potential Impact of Corrosion on the Ground Function of
Degradation of the High Pressure Injection Thermal
                              Electrical Conduit in Containment
Sleeves  
05000346/2002012-03     URI Potential Failure to Follow the Procedure for Raychem'
05000346/2002012-02
                              Splice Removal on Electrical Cables
URI
05000346/2002014-01c     URI Failure to Perform Comprehensive Moderate Energy Line
Potential Impact of Corrosion on the Ground Function of
                              Break Analysis
Electrical Conduit in Containment
05000346/2002014-01d     URI Lifting of Service Water Relief Valves
05000346/2002012-03
05000346/2002014-01e     URI Inadequate Service Water Pump Room Temperature
URI
                              Analysis
Potential Failure to Follow the Procedure for Raychem'
05000346/2002014-01f     URI Inadequate Service Water Pump Room Steam Line Break
Splice Removal on Electrical Cables
                              Analysis
05000346/2002014-01c
05000346/2002014-01g     URI Inadequate Cable Ampacity Analysis
URI
05000346/2002014-01h     URI Inadequate Flooding Protection for Service Water Pump
Failure to Perform Comprehensive Moderate Energy Line
                              House
Break Analysis
05000346/2002014-01j     URI Poor Quality Calculation for 90 Percent Undervoltage
05000346/2002014-01d
                              Relays
URI
05000346/2002014-01l     URI Inadequate Calculations for Control Room Operator Dose
Lifting of Service Water Relief Valves
                              (GDC-19) and Offsite Dose (10 CFR Part 100) Related to
05000346/2002014-01e
                              High Pressure Injection (HPI) Pump Minimum Flow Values
URI
05000346/2002014-01m     URI Other GDC-19 and 10 CFR Part 100 Issues
Inadequate Service Water Pump Room Temperature
05000346/2002014-01n     URI High Pressure Injection Pump Operation Under Long Term
Analysis
                              Minimum Flow
05000346/2002014-01f
05000346/2002014-01o     URI Some Small Break Loss of Coolant Accident Sizes Not
URI
                              Analyzed
Inadequate Service Water Pump Room Steam Line Break
05000346/2002014-01p     URI Inadequate Service Water System Flow Analysis
Analysis
                                        A4                                  Attachment
05000346/2002014-01g
URI
Inadequate Cable Ampacity Analysis
05000346/2002014-01h
URI
Inadequate Flooding Protection for Service Water Pump
House
05000346/2002014-01j
URI
Poor Quality Calculation for 90 Percent Undervoltage
Relays
05000346/2002014-01l
URI
Inadequate Calculations for Control Room Operator Dose
(GDC-19) and Offsite Dose (10 CFR Part 100) Related to
High Pressure Injection (HPI) Pump Minimum Flow Values
05000346/2002014-01m
URI
Other GDC-19 and 10 CFR Part 100 Issues
05000346/2002014-01n
URI
High Pressure Injection Pump Operation Under Long Term
Minimum Flow
05000346/2002014-01o
URI
Some Small Break Loss of Coolant Accident Sizes Not
Analyzed
05000346/2002014-01p
URI
Inadequate Service Water System Flow Analysis


              LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
05000346/2002014-01q     URI Inadequate Service Water System Thermal Analyses
Attachment
05000346/2002014-01r     URI Inadequate Ultimate Heat Sink Inventory Analysis
A5
05000346/2002014-01s     URI No Valid Service Water Pump Net Positive Suction Head
05000346/2002014-01q
                              Analysis
URI
05000346/2002014-01t     URI Service Water Source Temperature Analysis for Auxiliary
Inadequate Service Water System Thermal Analyses
                              Feedwater
05000346/2002014-01r
05000346/2002014-01u     URI Inadequate Short Circuit Calculations
URI
05000346/2002014-02b     URI Inadequate Service Water System Flow Balance Testing
Inadequate Ultimate Heat Sink Inventory Analysis
05000346/2002014-03a     URI Inappropriate Service Water Pump Curve Allowable
05000346/2002014-01s
                              Degradation
URI
05000346/2002014-03b     URI Repetitive Failures of Service Water Relief Valves
No Valid Service Water Pump Net Positive Suction Head
05000346/2002014-03c     URI Non-conservative Difference in Ultimate Heat Sink
Analysis
                              Temperature Measurements
05000346/2002014-01t
05000346/2002014-03e     URI Non-conservative Containment Air Cooler Mechanical
URI
                              Stress Analysis
Service Water Source Temperature Analysis for Auxiliary
05000346/2002014-05     URI Question Regarding the Definition of a Passive Failure
Feedwater
05000346/2002019-031     URI Final Evaluation of Apparent Cause Evaluation for LER
05000346/2002014-01u
                              05000346/2002-06-00
URI
05000346/2003-03-00     LER Potential Inadequate High Pressure Injection Pump
Inadequate Short Circuit Calculations
and -01                       Minimum Recirculation Flow Following a Small Break Loss
05000346/2002014-02b
                              of Coolant Accident
URI
Inadequate Service Water System Flow Balance Testing
05000346/2002014-03a
URI
Inappropriate Service Water Pump Curve Allowable
Degradation
05000346/2002014-03b
URI
Repetitive Failures of Service Water Relief Valves
05000346/2002014-03c
URI
Non-conservative Difference in Ultimate Heat Sink
Temperature Measurements
05000346/2002014-03e
URI
Non-conservative Containment Air Cooler Mechanical
Stress Analysis
05000346/2002014-05
URI
Question Regarding the Definition of a Passive Failure
05000346/2002019-031
URI
Final Evaluation of Apparent Cause Evaluation for LER
05000346/2002-06-00
05000346/2003-03-00
LER
Potential Inadequate High Pressure Injection Pump
and -01
Minimum Recirculation Flow Following a Small Break Loss
of Coolant Accident
Discussed
Discussed
05000346/2002-08-00     LER Containment Air Coolers Collective Significance of
05000346/2002-08-00
and -01                       Degraded Conditions
LER
05000346/2002014-01a     NCV Lack of a Design Basis Analysis for Containment Isolation
Containment Air Coolers Collective Significance of
                              Valve Backup Air Supplies
and -01
05000346/2002014-01b     NCV Inadequate Blowdown Provisions for CAC Backup Air
Degraded Conditions
                              Accumulators
05000346/2002014-01a
                                        A5                                    Attachment
NCV
Lack of a Design Basis Analysis for Containment Isolation
Valve Backup Air Supplies
05000346/2002014-01b
NCV
Inadequate Blowdown Provisions for CAC Backup Air
Accumulators


              LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont
05000346/2002014-01i     NCV Non-conservative TS Value for 90 Percent Undervoltage
Attachment
                              Relays
A6
05000346/2002014-01k     NCV Non-conservative Relay Setpoint Calculation for the 59
05000346/2002014-01i
                              Percent Undervoltage Relays
NCV
05000346/2002014-01v     NCV No Analytical Basis for Setpoint to Swap Service Water
Non-conservative TS Value for 90 Percent Undervoltage
                              System Discharge Path
Relays
05000346/2002014-02a     NCV SW Surveillance Test Did Not Use Worst Case Values
05000346/2002014-01k
05000346/2002014-03d     NCV Inadequate Corrective Actions Related to SW Pump
NCV
                              Discharge Check Valve Acceptance Criteria
Non-conservative Relay Setpoint Calculation for the 59
05000346/2002014-04     NCV Failure to Perform TS Surveillance Requirement for HPI
Percent Undervoltage Relays
                              Pump Following Maintenance
05000346/2002014-01v
05000346/2003016-01     AV   Reactor Operation with Pressure Boundary Leakage (URI
NCV
                              05000346/2002008-01)
No Analytical Basis for Setpoint to Swap Service Water
05000346/2003016-02     AV   Reactor Vessel Head Boric Acid Deposits (URI
System Discharge Path
                              05000346/2002008-02)
05000346/2002014-02a
05000346/2003016-03     AV   Containment Air Cooler Boric Acid Deposits (URI
NCV
                              05000346/2002008-03)
SW Surveillance Test Did Not Use Worst Case Values
05000346/2003016-04     AV   Radiation Element Filters (URI 05000346/2002008-04)
05000346/2002014-03d
05000346/2003016-05     AV   Service Structure Modification Delay (URI
NCV
                              05000346/2002008-05)
Inadequate Corrective Actions Related to SW Pump
05000346/2003016-06     AV   Reactor Coolant System Unidentified Leakage Trend (URI
Discharge Check Valve Acceptance Criteria
                              05000346/2002008-06)
05000346/2002014-04
05000346/2003016-07     AV   Inadequate Boric Acid Corrosion Control Program
NCV
                              Procedure (URI 05000346/2002008-07)
Failure to Perform TS Surveillance Requirement for HPI
05000346/2003016-08     AV   Failure to Follow Boric Acid Corrosion Control Program
Pump Following Maintenance
                              Procedure (URI 05000346/2002008-08)
05000346/2003016-01
05000346/2003016-09     AV   Failure to Follow Corrective Action Program Procedure
AV
                              (URI 05000346/2002008-09)
Reactor Operation with Pressure Boundary Leakage (URI
                                        A6                                    Attachment
05000346/2002008-01)
05000346/2003016-02
AV
Reactor Vessel Head Boric Acid Deposits (URI
05000346/2002008-02)
05000346/2003016-03
AV
Containment Air Cooler Boric Acid Deposits (URI
05000346/2002008-03)
05000346/2003016-04
AV
Radiation Element Filters (URI 05000346/2002008-04)
05000346/2003016-05
AV
Service Structure Modification Delay (URI
05000346/2002008-05)
05000346/2003016-06
AV
Reactor Coolant System Unidentified Leakage Trend (URI
05000346/2002008-06)
05000346/2003016-07
AV
Inadequate Boric Acid Corrosion Control Program
Procedure (URI 05000346/2002008-07)
05000346/2003016-08
AV
Failure to Follow Boric Acid Corrosion Control Program
Procedure (URI 05000346/2002008-08)
05000346/2003016-09
AV
Failure to Follow Corrective Action Program Procedure
(URI 05000346/2002008-09)


                                  LIST OF DOCUMENTS REVIEWED
Attachment
A7
LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC team reviewed the documents in their entirety but rather that selected
not imply that the NRC team reviewed the documents in their entirety but rather that selected
Line 5,618: Line 6,326:
of it, unless this is stated in the body of the inspection report.
of it, unless this is stated in the body of the inspection report.
Bulletins
Bulletins
        88-04; Potential Safety-Related Pump Loss; May 5, 1988
88-04; Potential Safety-Related Pump Loss; May 5, 1988
        03-01; Potential Impact of Debris Blockage on Emergency Sump Recirculation at
03-01; Potential Impact of Debris Blockage on Emergency Sump Recirculation at
        Pressurized-Water Reactor; June 9, 2003
Pressurized-Water Reactor; June 9, 2003
Calculations
Calculations
        C-CSS-009.03-002; Assessment of Safety Related Structures from the Effects of Intake
C-CSS-009.03-002; Assessment of Safety Related Structures from the Effects of Intake
        Structure Gantry Fall During a Tornado Event; Revision 0
Structure Gantry Fall During a Tornado Event; Revision 0
        C-CSS-099.20-026; Probability of Tornado Missile Damage to Davis-Besse Missile
C-CSS-099.20-026; Probability of Tornado Missile Damage to Davis-Besse Missile
        Exposed Targets; Revision 1; January 6, 2003
Exposed Targets; Revision 1; January 6, 2003
        C-EE-002.01-010; Battery Load Profile; Revision 29; September 18, 2002
C-EE-002.01-010; Battery Load Profile; Revision 29; September 18, 2002
        C-EE-004.01-049; 4.16 kV Bus Degraded (90 Percent Undervoltage) Relay Setpoint
C-EE-004.01-049; 4.16 kV Bus Degraded (90 Percent Undervoltage) Relay Setpoint
        Relay Setting Table Bus C1; Revision 2
Relay Setting Table Bus C1; Revision 2
        C-EE-004.01-049; 4.16 kV Bus Degraded (90 Percent Undervoltage) Relay Setpoint
C-EE-004.01-049; 4.16 kV Bus Degraded (90 Percent Undervoltage) Relay Setpoint
        Relay Setting Table Bus D1; Revision 7
Relay Setting Table Bus D1; Revision 7
        C-EE-015.03-008; Electric Transient Analysis Profile; Revisions 0 and 2
C-EE-015.03-008; Electric Transient Analysis Profile; Revisions 0 and 2
        C-EE-024.01-008; Evaluation of Davis-Besse EDG Voltage Frequency Response During
C-EE-024.01-008; Evaluation of Davis-Besse EDG Voltage Frequency Response During
        Design Basis LOOP/LOCA Transient Loading MPR 0200-0049-08-01; Revision 1
Design Basis LOOP/LOCA Transient Loading MPR 0200-0049-08-01; Revision 1
        C-ICE-011.01-002; Service Water Flow/Pressure Indications; Revision 0
C-ICE-011.01-002; Service Water Flow/Pressure Indications; Revision 0
        C-ICE-048.01-004; SFAS BWST Low Level Setpoint; Revision 7; April 22, 2003
C-ICE-048.01-004; SFAS BWST Low Level Setpoint; Revision 7; April 22, 2003
        C-ME-011.01-131; Service Water Relief Valve Setpoint and Capacity; Revision 0;
C-ME-011.01-131; Service Water Relief Valve Setpoint and Capacity; Revision 0;
        Addendum A01
Addendum A01
        C-ME-011.01-137; Service Water Pump NPSH; Revision 0
C-ME-011.01-137; Service Water Pump NPSH; Revision 0
        C-ME-011.01-140; SW/CCW Makeup Line 1 HBC-35 Flow Rate; Revision 0;
C-ME-011.01-140; SW/CCW Makeup Line 1 HBC-35 Flow Rate; Revision 0;
        March 6, 2003
March 6, 2003
                                                  A7                                  Attachment


Attachment
A8
C-ME-011.06-007; Accumulator Sizing for Service Water Valves SW1356, SW1357 and
C-ME-011.06-007; Accumulator Sizing for Service Water Valves SW1356, SW1357 and
SW1358; Revisions 0, 1, and 2
SW1358; Revisions 0, 1, and 2
Line 5,673: Line 6,382:
Revision 3; October 20, 2001
Revision 3; October 20, 2001
C-NSA-060.05-010; Containment Analysis; Revision 2; February 1, 2003
C-NSA-060.05-010; Containment Analysis; Revision 2; February 1, 2003
                                        A8                              Attachment


Attachment
A9
E-ECS-099.16-146; Thermal Aging Effect of ECCS Room Post LOCA Temperature;
E-ECS-099.16-146; Thermal Aging Effect of ECCS Room Post LOCA Temperature;
Revision 0; February 26, 1992
Revision 0; February 26, 1992
Line 5,704: Line 6,414:
August 30, 2002
August 30, 2002
86-5007079-00; SG Over-Pressure Protection Report; Revision 0
86-5007079-00; SG Over-Pressure Protection Report; Revision 0
                                      A9                                  Attachment


      86-5022260-00; Determination of HPI Pump Operability During Post-LOCA Sump
Attachment
      Recirculation For All Break Sizes And Transient Scenarios; Revision 0
A10
      86-5024418-01; DB-1 Post-LOCA pH Analysis Report; Revision 0
86-5022260-00; Determination of HPI Pump Operability During Post-LOCA Sump
Recirculation For All Break Sizes And Transient Scenarios; Revision 0
86-5024418-01; DB-1 Post-LOCA pH Analysis Report; Revision 0
Condition Reports Generated as a Result of this Inspection
Condition Reports Generated as a Result of this Inspection
      03-02191; Corrective Action Approval Without Supporting Documentation Finalized;
03-02191; Corrective Action Approval Without Supporting Documentation Finalized;
      March 19, 2003
March 19, 2003
      03-02195; Ambiguous Description in CRA No.8 to CR 02-07646; March 19, 2003
03-02195; Ambiguous Description in CRA No.8 to CR 02-07646; March 19, 2003
      03-02298; Failure to Generate CR for Unresolved Issues in NRC Inspection Report;
03-02298; Failure to Generate CR for Unresolved Issues in NRC Inspection Report;
      March 19, 2003
March 19, 2003
      03-02445; Incorrect Processing of CR 02-09928 and CR 02-0939; March 27, 2003
03-02445; Incorrect Processing of CR 02-09928 and CR 02-0939; March 27, 2003
      03-02475; Inadequate Blowdown Provisions for CAC Air Accumulators; March 28, 2003
03-02475; Inadequate Blowdown Provisions for CAC Air Accumulators; March 28, 2003
      03-02577; Appendix R Safe-Shutdown Concerns with EDG Floor Drains; April 1, 2003
03-02577; Appendix R Safe-Shutdown Concerns with EDG Floor Drains; April 1, 2003
      03-02597; Bypassed Overload Heaters in Class 1E 480V Motors; April 2, 2003
03-02597; Bypassed Overload Heaters in Class 1E 480V Motors; April 2, 2003
      03-02616; RFA - Bypassing Overload Heater Trips on 1E 480V Motors; April 2, 2003
03-02616; RFA - Bypassing Overload Heater Trips on 1E 480V Motors; April 2, 2003
      03-02651; Framatome AFW Issues with MSSV; April 3, 2003
03-02651; Framatome AFW Issues with MSSV; April 3, 2003
      03-02654; Cable Ampacity on Containment Spray Pump Motor; April 2, 2003
03-02654; Cable Ampacity on Containment Spray Pump Motor; April 2, 2003
      03-02730; Lack of Vendor Data for High Voltage Switchgear at High Temperature;
03-02730; Lack of Vendor Data for High Voltage Switchgear at High Temperature;
      March 19, 2003
March 19, 2003
      03-03184; Administrative Issues with CR 02-05640; April 25, 2003
03-03184; Administrative Issues with CR 02-05640; April 25, 2003
      03-03572; Lack of Coordination of Protective Devices on Bus E1 and F1; May 7, 2003
03-03572; Lack of Coordination of Protective Devices on Bus E1 and F1; May 7, 2003
      03-03891; EDG Room Heater Non-Q Yet Credited in USAR; May 19, 2003
03-03891; EDG Room Heater Non-Q Yet Credited in USAR; May 19, 2003
      03-03977; SW Calculations Do Not Provide Sufficient Documentation of Results;
03-03977; SW Calculations Do Not Provide Sufficient Documentation of Results;
      May 22, 2003
May 22, 2003
      03-03979; CR 02-00891 CA-30 Operation Confidence Review Closed Out Early;
03-03979; CR 02-00891 CA-30 Operation Confidence Review Closed Out Early;
      May 22, 2003
May 22, 2003
      03-03980; Past CAC Operability Determination Lacks Adequate Technical Justification;
03-03980; Past CAC Operability Determination Lacks Adequate Technical Justification;
      May 22, 2003
May 22, 2003
      03-03986; Rating of the Containment Air Cooler Fan Motors; May 22, 2003
03-03986; Rating of the Containment Air Cooler Fan Motors; May 22, 2003
                                            A10                                Attachment


Attachment
A11
03-04010; NRC Review of SW/CCW Interface Calculation; May 22, 2003
03-04010; NRC Review of SW/CCW Interface Calculation; May 22, 2003
03-04018; NRC Pointed out Discrepancy in Mode Hold Resolution for CR 02-01523;
03-04018; NRC Pointed out Discrepancy in Mode Hold Resolution for CR 02-01523;
Line 5,766: Line 6,478:
03-06153; Timeliness of Changes to the USAR; July 31, 2003
03-06153; Timeliness of Changes to the USAR; July 31, 2003
03-06338; Discrepancies in CR 02-06773 Response; August 8, 2003
03-06338; Discrepancies in CR 02-06773 Response; August 8, 2003
                                      A11                                  Attachment


Attachment
A12
03-06375; Concerns with Motor Overload Protection for Non-Essential Service Motors;
03-06375; Concerns with Motor Overload Protection for Non-Essential Service Motors;
August 8, 2003
August 8, 2003
Line 5,780: Line 6,493:
03-06428; Lack of Corrective Action for Cause Identification CR 02-09027 Self-Identified
03-06428; Lack of Corrective Action for Cause Identification CR 02-09027 Self-Identified
In Preparation for Inspection; August 9, 2003
In Preparation for Inspection; August 9, 2003
03-06457; Discrepancies Between Quality and Seismic Classifications;
03-06457; Discrepancies Between Quality and Seismic Classifications;  
August 11, 2003
August 11, 2003
03-06458; Invalid Information Restored to Procedure During Alteration Self-Identified In
03-06458; Invalid Information Restored to Procedure During Alteration Self-Identified In
Line 5,799: Line 6,512:
August 13, 2003
August 13, 2003
03-06524; EDG Conduit Installation for Cabinet C3615; August 2, 2003
03-06524; EDG Conduit Installation for Cabinet C3615; August 2, 2003
                                        A12                                  Attachment


Attachment
A13
03-06526; Adequacy of HPI Pump Minimum Flow Rate; August 13, 2003
03-06526; Adequacy of HPI Pump Minimum Flow Rate; August 13, 2003
03-06547; Potential for Supervisor/SRO Comments to Influence CR Outcome;
03-06547; Potential for Supervisor/SRO Comments to Influence CR Outcome;
Line 5,830: Line 6,544:
03-06944; Fuse Sizing for MV0106 and MV38700; August 25, 2003
03-06944; Fuse Sizing for MV0106 and MV38700; August 25, 2003
03-06948; Downgrade of CR 02-06356; August 26, 2003
03-06948; Downgrade of CR 02-06356; August 26, 2003
                                      A13                                  Attachment


Attachment
A14
03-06956; 0300 - DC Voltage Drop LC - Lack of Basis for Deferring Corrective Action;
03-06956; 0300 - DC Voltage Drop LC - Lack of Basis for Deferring Corrective Action;
August 26, 2003
August 26, 2003
Line 5,862: Line 6,577:
03-07256; Questions on Applicability of 50.59 for Manual Actions in Fire Preplans;
03-07256; Questions on Applicability of 50.59 for Manual Actions in Fire Preplans;
September 2, 2003
September 2, 2003
                                      A14                                    Attachment


      03-07420; Restart CRs Closed Prior to All CAs Being Completed; September 6, 2003
Attachment
      03-07922; Thermal Overload #2 EDG Air Compressor; September 21, 2003
A15
      03-09548; New Motor Operated Valve Terminal Voltage; November 5, 2003
03-07420; Restart CRs Closed Prior to All CAs Being Completed; September 6, 2003
03-07922; Thermal Overload #2 EDG Air Compressor; September 21, 2003
03-09548; New Motor Operated Valve Terminal Voltage; November 5, 2003
Condition Reports Reviewed During the Inspection
Condition Reports Reviewed During the Inspection
      99-01109; Conversion of PCAQR 1998-0126 to Condition Report; June 28, 1999
99-01109; Conversion of PCAQR 1998-0126 to Condition Report; June 28, 1999
      00-00669; Potential Non-Compliance Against the ASME Code; April 1, 2000
00-00669; Potential Non-Compliance Against the ASME Code; April 1, 2000
      00-00699; Steady State Leakage from Three of Four Reactor Coolant Pump Gasket
00-00699; Steady State Leakage from Three of Four Reactor Coolant Pump Gasket
      Drain Lines; April 2, 2000
Drain Lines; April 2, 2000
      00-00869; Leakage at the Bolted Connection on Reactor Coolant Pump 1-1;
00-00869; Leakage at the Bolted Connection on Reactor Coolant Pump 1-1;
      April 10, 2000
April 10, 2000
      00-01089; Relaxation of Reactor Coolant Pump Casing Studs since Refueling Outage
00-01089; Relaxation of Reactor Coolant Pump Casing Studs since Refueling Outage
      11; April 20, 2000
11; April 20, 2000
      00-02033; Reactor Coolant System Flow Rate Test Acceptance Criteria Not Met;
00-02033; Reactor Coolant System Flow Rate Test Acceptance Criteria Not Met;
      August 11, 2000
August 11, 2000
      00-02304; Performance of DB-SP-04360 In Modes 1 and 2; September 21, 2000
00-02304; Performance of DB-SP-04360 In Modes 1 and 2; September 21, 2000
      00-02418; Zebra Mussel Particles in Service Water Lines Might Restrict Flow Through
00-02418; Zebra Mussel Particles in Service Water Lines Might Restrict Flow Through
      the Auxiliary Feedwater Restriction Orifices; October 6, 2000
the Auxiliary Feedwater Restriction Orifices; October 6, 2000
      01-00540; Dose Calculations for Post Accident Sampling System Samples Outside of
01-00540; Dose Calculations for Post Accident Sampling System Samples Outside of
      Updated Safety Analysis Report 9.3.2.2.3; February 23, 2001
Updated Safety Analysis Report 9.3.2.2.3; February 23, 2001
      01-00890; Reactor Coolant System Leak Rate Data Scatter; March 28, 2001
01-00890; Reactor Coolant System Leak Rate Data Scatter; March 28, 2001
      01-01102; Letdown Diverting Valve, MU11, Is Possible Source of Reactor Coolant
01-01102; Letdown Diverting Valve, MU11, Is Possible Source of Reactor Coolant
      System Unidentified Leakage; April 20, 2001
System Unidentified Leakage; April 20, 2001
      01-01335; CAC Air Side Fouling Criteria; May 22, 2001
01-01335; CAC Air Side Fouling Criteria; May 22, 2001
      01-01857; RCS Leakage Anomalies; July 25, 2001
01-01857; RCS Leakage Anomalies; July 25, 2001
      01-02019; Initial Results of Investigation into NRC Information Notice 2000-20;
01-02019; Initial Results of Investigation into NRC Information Notice 2000-20;
      August 7, 2001
August 7, 2001
      01-02820; Procedures Not Updated to Support Modification Implementation;
01-02820; Procedures Not Updated to Support Modification Implementation;
      October 23, 2001
October 23, 2001
      01-02862; Potential Adverse Trend in Unidentified Reactor Coolant System Leakage;
01-02862; Potential Adverse Trend in Unidentified Reactor Coolant System Leakage;
      October 25, 2001
October 25, 2001
                                                A15                                Attachment


Attachment
A16
01-03025; Reactor Coolant System Leakage; November 12, 2001
01-03025; Reactor Coolant System Leakage; November 12, 2001
01-03059; Minimum Voltage for AFW Valves MV0106 and MV3870; November 2001
01-03059; Minimum Voltage for AFW Valves MV0106 and MV3870; November 2001
Line 5,926: Line 6,643:
June 13, 2002
June 13, 2002
02-02658; Inadequate Ventilation for Rooms 323, 324 and 325
02-02658; Inadequate Ventilation for Rooms 323, 324 and 325
                                        A16                                  Attachment


Attachment
A17
02-02848; Fuel Assembly Spacer Grid Impressions in Core Baffle Plates; June 27, 2002
02-02848; Fuel Assembly Spacer Grid Impressions in Core Baffle Plates; June 27, 2002
02-02943; Containment Air Cooler Boric Acid Corrosion; July 2, 2002
02-02943; Containment Air Cooler Boric Acid Corrosion; July 2, 2002
Line 5,937: Line 6,655:
02-03497; Overall Failure to Take Action to Correct Identified Deficiencies in CAP;
02-03497; Overall Failure to Take Action to Correct Identified Deficiencies in CAP;
July 27, 2002
July 27, 2002
02-03674; Recurring Trend of Untimely and Ineffective Corrective Actions;
02-03674; Recurring Trend of Untimely and Ineffective Corrective Actions;  
August 3, 2002
August 3, 2002
02-03668; Reactor Coolant Pump Casing-to-cover Joint Leakage; August 3, 2002
02-03668; Reactor Coolant Pump Casing-to-cover Joint Leakage; August 3, 2002
Line 5,956: Line 6,674:
02-04630; LIR - Emergency Diesel Generator 1-2; August 18, 2002
02-04630; LIR - Emergency Diesel Generator 1-2; August 18, 2002
02-04668; LIR - AFW-EQ Equipment Sealing; August 21, 2002
02-04668; LIR - AFW-EQ Equipment Sealing; August 21, 2002
                                      A17                                      Attachment


Attachment
A18
02-04673; Auxiliary Feedwater Strainers Limiting Particle Size; August 22, 2002
02-04673; Auxiliary Feedwater Strainers Limiting Particle Size; August 22, 2002
02-04680; No Documentation To Assure Compliance With GE SIL-44 For HFAs;
02-04680; No Documentation To Assure Compliance With GE SIL-44 For HFAs;
Line 5,987: Line 6,706:
August 30, 2002
August 30, 2002
02-05356; Service Water Technical Specification Instruments; September 10, 2002
02-05356; Service Water Technical Specification Instruments; September 10, 2002
                                      A18                                  Attachment


Attachment
A19
02-05364; LIR - EDG Electrical Capacity C-EE-024.01-005, R8, is to Be Revised;
02-05364; LIR - EDG Electrical Capacity C-EE-024.01-005, R8, is to Be Revised;
September 3, 2002
September 3, 2002
Line 6,020: Line 6,740:
02-05640; LIR - No Design Bases/Flow Verification Testing of SW Flow to AFW
02-05640; LIR - No Design Bases/Flow Verification Testing of SW Flow to AFW
System; September 10, 2002
System; September 10, 2002
                                      A19                                  Attachment


Attachment
A20
02-05645; Fuel Assembly NJ10KK Spacer Grid Damage; September 6, 2002
02-05645; Fuel Assembly NJ10KK Spacer Grid Damage; September 6, 2002
02-05691; LIR - Minimum Temperature to the AFW System SG Nozzles;
02-05691; LIR - Minimum Temperature to the AFW System SG Nozzles;
Line 6,052: Line 6,773:
02-05925; LIR - EDG Transient Analysis During Loading Sequence - Calculations;
02-05925; LIR - EDG Transient Analysis During Loading Sequence - Calculations;
September 12, 2002
September 12, 2002
                                      A20                                Attachment


Attachment
A21
02-05986; Ultimate Heat Sink Water Inventory Analysis Does Not Consider All Water
02-05986; Ultimate Heat Sink Water Inventory Analysis Does Not Consider All Water
Losses; September 14, 2002
Losses; September 14, 2002
02-06062; LIR - EDG: Fuel Filter Inlet Operating Pressure Exceeds Vendor Limits for
02-06062; LIR - EDG: Fuel Filter Inlet Operating Pressure Exceeds Vendor Limits for
Change; September 14, 2002
Change; September 14, 2002
02-06064; SSDI Item - SW Flow Balance Margins and Need for Additional Recorded
02-06064; SSDI Item - SW Flow Balance Margins and Need for Additional Recorded
Line 6,073: Line 6,795:
02-06215; Excessive Indicated Total RCS Flow Error in SP-03358; September 18, 2002
02-06215; Excessive Indicated Total RCS Flow Error in SP-03358; September 18, 2002
02-06275; Degraded Makeup Valve MU11 Hardware; September 19, 2002
02-06275; Degraded Makeup Valve MU11 Hardware; September 19, 2002
02-06305; SSDI Item - C-EE-015.03-003, Steady-State Analysis: ELMS;
02-06305; SSDI Item - C-EE-015.03-003, Steady-State Analysis: ELMS;
September 19, 2002
September 19, 2002
02-06333; Inadequate SW Thermal Analysis; September 19, 2002
02-06333; Inadequate SW Thermal Analysis; September 19, 2002
02-06337; SSDI Item - SW C-NSA-011.01-007, Revision 1 Concerns (Pump Curves);
02-06337; SSDI Item - SW C-NSA-011.01-007, Revision 1 Concerns (Pump Curves);
September 19, 2002
September 19, 2002
02-06341; LIR - SW: Review of Industry Experience; September 20, 2002
02-06341; LIR - SW: Review of Industry Experience; September 20, 2002
02-06343; Nuclear Quality Assurance Stop Work on Nuclear Fuel Movements;
02-06343; Nuclear Quality Assurance Stop Work on Nuclear Fuel Movements;
September 20, 2002
September 20, 2002
Line 6,084: Line 6,806:
02-06370; SSDI Item - ECCS Pump Room Heat Load is Non-conservative;
02-06370; SSDI Item - ECCS Pump Room Heat Load is Non-conservative;
September 20, 2002
September 20, 2002
                                      A21                                Attachment


Attachment
A22
02-06384; SSDI Item - Enhancement to Calculation 50.20 Flooding of ECCS Rooms
02-06384; SSDI Item - Enhancement to Calculation 50.20 Flooding of ECCS Rooms
Due to a Feedwater Line Break; September 20, 2002
Due to a Feedwater Line Break; September 20, 2002
Line 6,094: Line 6,817:
02-06477; SSDI Item - HPI Pump Performance Not Evaluated For Expected Input
02-06477; SSDI Item - HPI Pump Performance Not Evaluated For Expected Input
Power Variations; September 2002
Power Variations; September 2002
02-06536; LIR - RCS: PZR Vent Flow Capacity Has No Design Basis; September 2002
02-06536; LIR - RCS: PZR Vent Flow Capacity Has No Design Basis; September 2002
02-06547; Design Basis Validation - Pressurizer Vent Orifice Sizing; September 2002
02-06547; Design Basis Validation - Pressurizer Vent Orifice Sizing; September 2002
02-06564; Service Water System Cleanliness for Restart; October 5, 2002
02-06564; Service Water System Cleanliness for Restart; October 5, 2002
Line 6,115: Line 6,838:
02-06860; Review of the Need for Relief Valves for Several Heat Exchangers;
02-06860; Review of the Need for Relief Valves for Several Heat Exchangers;
September 27, 2002
September 27, 2002
                                      A22                                  Attachment


Attachment
A23
02-06861; Bearing Oil Cooler Strainer Fouling; September 27, 2002
02-06861; Bearing Oil Cooler Strainer Fouling; September 27, 2002
02-06885; Reactor Coolant System Flow Uncertainty May Be Higher than Assumed;
02-06885; Reactor Coolant System Flow Uncertainty May Be Higher than Assumed;
Line 6,132: Line 6,856:
Capacity; October 1, 2002
Capacity; October 1, 2002
02-07236; LIR - AFW SG Accident Pressure versus AFW Pump Flow; October 1, 2002
02-07236; LIR - AFW SG Accident Pressure versus AFW Pump Flow; October 1, 2002
02-07278; RC2 Pressurizer Spray Valve Design; October 1, 2002
02-07278; RC2 Pressurizer Spray Valve Design; October 1, 2002
02-07328; Lack of Timeliness for Radiation Protection Action Implementation;
02-07328; Lack of Timeliness for Radiation Protection Action Implementation;
October 3, 2002
October 3, 2002
Line 6,144: Line 6,868:
02-07516; LIR - CAC SW Flow Tests Indicate Adverse Trend; September 9, 2002
02-07516; LIR - CAC SW Flow Tests Indicate Adverse Trend; September 9, 2002
02-07524; LIR - AFW Pump Curves; October 2002
02-07524; LIR - AFW Pump Curves; October 2002
02-07559; LIR - RCS: Lack of Response to Request For Assistance for Design Basis
02-07559; LIR - RCS: Lack of Response to Request For Assistance for Design Basis
Validation Information; October 2002
Validation Information; October 2002
                                      A23                                  Attachment


Attachment
A24
02-07596; EDG High Temperature Overall; October 17, 2002
02-07596; EDG High Temperature Overall; October 17, 2002
02-07599; LIR - EDG High Temperature - Determine Capability to Function;
02-07599; LIR - EDG High Temperature - Determine Capability to Function;
Line 6,178: Line 6,903:
02-07781; Weaknesses in Testing Service Water Outlet Valves to Containment Air
02-07781; Weaknesses in Testing Service Water Outlet Valves to Containment Air
Coolers; October 9, 2002
Coolers; October 9, 2002
                                      A24                                  Attachment


Attachment
A25
02-07802; Basis for PSH 2929 and PSH 2930 Not Found; October 10, 2002
02-07802; Basis for PSH 2929 and PSH 2930 Not Found; October 10, 2002
02-07889; Open Item for Screen Wash and Service Water Systems; October 11, 2002
02-07889; Open Item for Screen Wash and Service Water Systems; October 11, 2002
Line 6,208: Line 6,934:
02-09928; HPI Thermal Sleeve 2-1 Degradation; December 2002
02-09928; HPI Thermal Sleeve 2-1 Degradation; December 2002
02-09947; Inadequate Tracking of Condition Report Rollovers; December 14, 2002
02-09947; Inadequate Tracking of Condition Report Rollovers; December 14, 2002
                                      A25                                  Attachment


Attachment
A26
02-10369; Condition Report Trend Analysis Not Performed Regularly;
02-10369; Condition Report Trend Analysis Not Performed Regularly;
December 19, 2002
December 19, 2002
Line 6,240: Line 6,967:
February 21, 2003
February 21, 2003
03-01492; Fuel Assembly NJ1271 Damaged Spacer Grid; February 24, 2003
03-01492; Fuel Assembly NJ1271 Damaged Spacer Grid; February 24, 2003
                                      A26                                  Attachment


      03-01648; Unacceptable SG Tube Stresses in Appendix R Cooldown;
Attachment
      February 28, 2003
A27
      03-01870; PR/BACC: CR/CA; March 8, 2003
03-01648; Unacceptable SG Tube Stresses in Appendix R Cooldown;  
      03-01955; CR Rollover Discrepancies; March 12, 2003
February 28, 2003
      03-02220; Emergency Diesel Generator Component Cooling Water Flows Inconsistent
03-01870; PR/BACC: CR/CA; March 8, 2003
      with Modification 97-0029 Requirements; March 20, 2003
03-01955; CR Rollover Discrepancies; March 12, 2003
      03-02699; DB-OP-02519 Does Not Match Plant Configuration; April 4, 2003
03-02220; Emergency Diesel Generator Component Cooling Water Flows Inconsistent
      03-05925; Weaknesses in Conduct of Trending; July 23, 2003
with Modification 97-0029 Requirements; March 20, 2003
      03-06296; Boric Acid Identified on Reactor Coolant Pump 2-2; August 5, 2003
03-02699; DB-OP-02519 Does Not Match Plant Configuration; April 4, 2003
      03-06655; Superceded Calculations Were Not Tracked According to EN-DP-0140;
03-05925; Weaknesses in Conduct of Trending; July 23, 2003
      August 18, 2003
03-06296; Boric Acid Identified on Reactor Coolant Pump 2-2; August 5, 2003
      03-07656; Forward Flow Rate of 10,000 Gpm Not Attained for SW19 During
03-06655; Superceded Calculations Were Not Tracked According to EN-DP-0140;
      DB-PB-03232; September 12, 2003
August 18, 2003
      03-08196; Mode 3A System Leakage Test; RCP 2-1 Boric Acid Deposits;
03-07656; Forward Flow Rate of 10,000 Gpm Not Attained for SW19 During
      September 26, 2003
DB-PB-03232; September 12, 2003
      03-08249, Classification of CR 02-05590 for LER 2002-006 on Tornado Missile
03-08196; Mode 3A System Leakage Test; RCP 2-1 Boric Acid Deposits;
      Protection; September 28, 2003
September 26, 2003
03-08249, Classification of CR 02-05590 for LER 2002-006 on Tornado Missile
Protection; September 28, 2003
Drawings
Drawings
      E-1037P; Electrical Grounding Details; Sheet 2; Revision 1
E-1037P; Electrical Grounding Details; Sheet 2; Revision 1
      E-1037P; Electrical Grounding Details; Sheet 3; Revision 1
E-1037P; Electrical Grounding Details; Sheet 3; Revision 1
      E-1037P; Electrical Grounding Details; Sheet 10; Revision 0
E-1037P; Electrical Grounding Details; Sheet 10; Revision 0
      E-1037P; Electrical Grounding Details; Sheet 11; Revision 0
E-1037P; Electrical Grounding Details; Sheet 11; Revision 0
      E-1042; Emergency Diesel Generator 1-1 Loading Table; Sheet 1; Revision14
E-1042; Emergency Diesel Generator 1-1 Loading Table; Sheet 1; Revision14
      E-1042; Emergency Diesel Generator 1-1 Loading Table; Sheet 2; Revision16
E-1042; Emergency Diesel Generator 1-1 Loading Table; Sheet 2; Revision16
      E-1043; Emergency Diesel Generator 1-2 Loading Table; Sheet 1; Revision 1 4
E-1043; Emergency Diesel Generator 1-2 Loading Table; Sheet 1; Revision 1 4
      E-1043; Emergency Diesel Generator 1-2 Loading Table; Sheet 2; Revision 15
E-1043; Emergency Diesel Generator 1-2 Loading Table; Sheet 2; Revision 15
      M-006D; Auxiliary Feedwater System; Revision 47
M-006D; Auxiliary Feedwater System; Revision 47
      M-017A; Diesel Generators; Revision 1
M-017A; Diesel Generators; Revision 1
                                            A27                                Attachment


      M-017C; Diesel Generators Fuel Oil; Revision 22
Attachment
      M-033A; High Pressure Injection; Revision 30
A28
      M-036A; Component Cooling Water System; Revision 24
M-017C; Diesel Generators Fuel Oil; Revision 22
      M-036B; Component Cooling Water System; Revision 30
M-033A; High Pressure Injection; Revision 30
      M-036C; Component Cooling Water System; Revision 25
M-036A; Component Cooling Water System; Revision 24
      M-041A; Service Water Pumps and Secondary Service Water System; Revision 25
M-036B; Component Cooling Water System; Revision 30
      M-041B; Primary Service Water System; Revision 54
M-036C; Component Cooling Water System; Revision 25
      M-041C; Service Water System for Containment Air Coolers; Revision 25
M-041A; Service Water Pumps and Secondary Service Water System; Revision 25
      M-096D; Auxiliary Feedwater System; Revision 47
M-041B; Primary Service Water System; Revision 54
      7749-M-508-74-8; Byron-Jackson Reactor Coolant Pump; Sheets 1 and 2; Revision D
M-041C; Service Water System for Containment Air Coolers; Revision 25
      7M-017B; Diesel Generators Air Start; Revision 32
M-096D; Auxiliary Feedwater System; Revision 47
7749-M-508-74-8; Byron-Jackson Reactor Coolant Pump; Sheets 1 and 2; Revision D
7M-017B; Diesel Generators Air Start; Revision 32
Engineering Change Packages and Requests
Engineering Change Packages and Requests
      99-0039-00; Replacement of Containment Air Cooler Service Water Discharge Valves;
99-0039-00; Replacement of Containment Air Cooler Service Water Discharge Valves;
      Revision 1
Revision 1
      01-0306A; At Risk Change: Component Cooling Water Heat Exchanger Bolt
01-0306A; At Risk Change: Component Cooling Water Heat Exchanger Bolt
      Replacement and Deletion of Relief Valves SW3962 and SW3963; April 18, 2003
Replacement and Deletion of Relief Valves SW3962 and SW3963; April 18, 2003
      01-0306B; At Risk Change: Component Cooling Water Heat Exchanger Bolt
01-0306B; At Risk Change: Component Cooling Water Heat Exchanger Bolt
      Replacement and Deletion of Relief Valves SW3962 and SW3963; April 22, 2003
Replacement and Deletion of Relief Valves SW3962 and SW3963; April 22, 2003
      03-0074-00; Install Larger Mesh in Strainer Baskets on Service Water Inlet to Auxiliary
03-0074-00; Install Larger Mesh in Strainer Baskets on Service Water Inlet to Auxiliary
      Feedwater Pumps and New Strainers Upstream of the Restricting Orifices;
Feedwater Pumps and New Strainers Upstream of the Restricting Orifices;
      June 19, 2003
June 19, 2003
      03-0243-00; Rewire the Control Circuitry for CAC Fan 1-1 Such That in the Case of a
03-0243-00; Rewire the Control Circuitry for CAC Fan 1-1 Such That in the Case of a
      Control Room Fire, This Fan Can Be Started in Slow Speed to Provide Cooling to the
Control Room Fire, This Fan Can Be Started in Slow Speed to Provide Cooling to the
      Containment; July 2003
Containment; July 2003
      03-0267-00; Provide Level and Pressure Indication for the Idle SG on the Auxiliary
03-0267-00; Provide Level and Pressure Indication for the Idle SG on the Auxiliary
      Shutdown Panel to Support Appendix R Safe Shutdown; July 2003
Shutdown Panel to Support Appendix R Safe Shutdown; July 2003
Engineering Work Requests
Engineering Work Requests
      01-0306-00; Remove Service Water Header Relief Valves; December 10, 2001
01-0306-00; Remove Service Water Header Relief Valves; December 10, 2001
                                            A28                                    Attachment


      01-0378-00; Provide Larger Access Holes to Enable Removal of Boric Acid;
Attachment
      August 30, 2001
A29
      02-0138-00; RV Service Structure Support Skirt Openings; April 11, 2002
01-0378-00; Provide Larger Access Holes to Enable Removal of Boric Acid;
      02-0217-00; Replace Existing Reactor Vessel Head; June 4, 2002
August 30, 2001
02-0138-00; RV Service Structure Support Skirt Openings; April 11, 2002
02-0217-00; Replace Existing Reactor Vessel Head; June 4, 2002
Evaluations
Evaluations
      Basic Cause Analysis Report for CR 02-09314
Basic Cause Analysis Report for CR 02-09314
      Root Cause Analysis for CR 03-00425
Root Cause Analysis for CR 03-00425
      Root Cause Analysis for CR 02-04673; March 18, 2003
Root Cause Analysis for CR 02-04673; March 18, 2003
      Root Cause Analysis for CR 02-06178; February 1, 2003
Root Cause Analysis for CR 02-06178; February 1, 2003
      Root Cause Analysis for CR 03-02597
Root Cause Analysis for CR 03-02597
      Operability Evaluation 02-0036; Tornado Missile Protection Issues; December 17, 2002
Operability Evaluation 02-0036; Tornado Missile Protection Issues; December 17, 2002
      Operability Evaluation 03-0009; Revision 1 for CR 03-00949
Operability Evaluation 03-0009; Revision 1 for CR 03-00949
Information Notices
Information Notices
      80-13; General Electric Type SBM Control Switches - Defective Cam Follower;
80-13; General Electric Type SBM Control Switches - Defective Cam Follower;
      April 4, 1980
April 4, 1980
      85-94; Potential for Loss of Minimum Flow Paths Leading to ECCS Pump Damage
85-94; Potential for Loss of Minimum Flow Paths Leading to ECCS Pump Damage
      During a LOCA; December 13, 1985
During a LOCA; December 13, 1985
      97-12; Potential Armature Binding in General Electric Type HGA Relays;
97-12; Potential Armature Binding in General Electric Type HGA Relays;
      March 24, 1977
March 24, 1977
      98-19; Shaft Binding in General Electric Type SBM Control Switches; June 3, 1978
98-19; Shaft Binding in General Electric Type SBM Control Switches; June 3, 1978
Inspection Manual Chapters
Inspection Manual Chapters
      0305; Operating Reactor Assessment Program; February 19, 2003
0305; Operating Reactor Assessment Program; February 19, 2003
      0350; Oversight of Operating Reactor Facilities in an Extended Shutdown as a Result of
0350; Oversight of Operating Reactor Facilities in an Extended Shutdown as a Result of
      Significant Performance Problems; March 6, 2001
Significant Performance Problems; March 6, 2001
      0609; Significance Determination Process; April 21, 2003
0609; Significance Determination Process; April 21, 2003
                Appendix A; Significance Determination of Reactor Inspection Findings for
Appendix A; Significance Determination of Reactor Inspection Findings for
                At-Power Situations; March 18, 2002
At-Power Situations; March 18, 2002
                                              A29                                  Attachment


                Appendix C; Occupational Radiation Safety Significance Determination Process;
Attachment
                June 24, 2003
A30
                Appendix D; Public Radiation Safety Significance Determination Process; July
Appendix C; Occupational Radiation Safety Significance Determination Process;
                24, 2003
June 24, 2003
                Appendix F; Fire Protection Significance Determination Process;
Appendix D; Public Radiation Safety Significance Determination Process; July
                February 27, 2001
24, 2003
                Appendix H (Draft) Containment Integrity Significance Determination Process;
Appendix F; Fire Protection Significance Determination Process;  
                July 8, 2003
February 27, 2001
      0612; Power Reactor Inspection Reports; June 20, 2003
Appendix H (Draft) Containment Integrity Significance Determination Process;
July 8, 2003
0612; Power Reactor Inspection Reports; June 20, 2003
Inspection Reports
Inspection Reports
      05000346/1995007; Routine Inspection Report; September 29, 1995
05000346/1995007; Routine Inspection Report; September 29, 1995
      05000346/1999001; Routine Inspection Report; March 5, 1999
05000346/1999001; Routine Inspection Report; March 5, 1999
      05000346/1999004; Routine Inspection Report; June 7, 1999
05000346/1999004; Routine Inspection Report; June 7, 1999
      05000346/2002003; Augmented Inspection Team - Degradation of the Reactor
05000346/2002003; Augmented Inspection Team - Degradation of the Reactor
      Pressure Vessel Head; May 3, 2002
Pressure Vessel Head; May 3, 2002
      05000346/2002012; Special Inspection - Boric Acid Corrosion Extent of Condition;
05000346/2002012; Special Inspection - Boric Acid Corrosion Extent of Condition;
      November 29, 2002
November 29, 2002
      05000346/2002014; Safety System Design and Performance Capability Inspection;
05000346/2002014; Safety System Design and Performance Capability Inspection;
      February 26, 2003
February 26, 2003
      05000346/2002017; Integrated Inspection Report; December 9, 2002
05000346/2002017; Integrated Inspection Report; December 9, 2002
      05000346/2002019; Integrated Inspection Report; January 31, 2003
05000346/2002019; Integrated Inspection Report; January 31, 2003
Intra-Company Memoranda
Intra-Company Memoranda
      NPE 01-00071; OE 12074 - Boric Acid Corrosion of Carbon Steel Components at the
NPE 01-00071; OE 12074 - Boric Acid Corrosion of Carbon Steel Components at the
      Reactor Coolant System Pressure Boundary; April 27, 2001
Reactor Coolant System Pressure Boundary; April 27, 2001
      NPE 02-00227; Reactor Coolant Pump Issues; August 9, 2002
NPE 02-00227; Reactor Coolant Pump Issues; August 9, 2002
      NPE 03-00047; Reactor Coolant Pump Status to August 9, 2002, White Paper;
NPE 03-00047; Reactor Coolant Pump Status to August 9, 2002, White Paper;
      April 3, 2003
April 3, 2003
Generic Letters
Generic Letters
      89-13; Service Water System Problems Affecting Safety-Related Equipment;
89-13; Service Water System Problems Affecting Safety-Related Equipment;  
      July 18, 1989 and Supplement 1; April 4, 1990
July 18, 1989 and Supplement 1; April 4, 1990
                                              A30                                  Attachment


        91-18; Information to Licensees Regarding Two NRC Inspection Manual Sections on
Attachment
        Resolution of Degraded and Non-Conforming Conditions and on Operability; Revision 1,
A31
        October 8, 1997
91-18; Information to Licensees Regarding Two NRC Inspection Manual Sections on
        96-06; Assurance of Equipment Operability And Containment Integrity During
Resolution of Degraded and Non-Conforming Conditions and on Operability; Revision 1,
        Design-Basis Accident Conditions; September 30, 1996 and Supplement 1; November
October 8, 1997
        13, 1997
96-06; Assurance of Equipment Operability And Containment Integrity During
Design-Basis Accident Conditions; September 30, 1996 and Supplement 1; November
13, 1997
Letters
Letters
        Amendment 33 to Facility Operating License NPF-3 for Davis-Besse Nuclear Power
Amendment 33 to Facility Operating License NPF-3 for Davis-Besse Nuclear Power
        Station Unit No.1, NRC to Toledo Edison; October 1, 1980
Station Unit No.1, NRC to Toledo Edison; October 1, 1980
        Amendment 45 to Facility Operating License NPF-3 Cycle 3 Operation, NRC to Toledo
Amendment 45 to Facility Operating License NPF-3 Cycle 3 Operation, NRC to Toledo
        Edison; July 28, 1982
Edison; July 28, 1982
        Amendment 80 to Facility Operating License NPF-3 Cycle 5 Operation, NRC to Toledo
Amendment 80 to Facility Operating License NPF-3 Cycle 5 Operation, NRC to Toledo
        Edison; December 13, 1984
Edison; December 13, 1984
        Component Cooling Water System, First Energy S/N 2949; May 21, 2003
Component Cooling Water System, First Energy S/N 2949; May 21, 2003
        Davis-Besse Nuclear Power Station, Unit 1 - Requests For Relief for the Third 10-year
Davis-Besse Nuclear Power Station, Unit 1 - Requests For Relief for the Third 10-year
        Interval Inservice Inspection Program Plan (TAC MB1607), NRC to First Energy;
Interval Inservice Inspection Program Plan (TAC MB1607), NRC to First Energy;
        September 30, 2002
September 30, 2002
        Davis-Besse Reactor Coolant Pump Casing Joint Analysis, Flowserve to First Energy;
Davis-Besse Reactor Coolant Pump Casing Joint Analysis, Flowserve to First Energy;
        April 24, 2003
April 24, 2003
        Davis-Besse Reactor Coolant Pump Shaft Bearing Cracking, MPR Associates to First
Davis-Besse Reactor Coolant Pump Shaft Bearing Cracking, MPR Associates to First
        Energy; February 7, 2003
Energy; February 7, 2003
        Evaluation of Ultimate Heat Sink Pond Thermal Performance, Bechtel to First Energy;
Evaluation of Ultimate Heat Sink Pond Thermal Performance, Bechtel to First Energy;
        May 19, 2002
May 19, 2002
        Exemption from Certain Requirements of Appendix R to 10 CFR Part 50, NRC to Toledo
Exemption from Certain Requirements of Appendix R to 10 CFR Part 50, NRC to Toledo
        Edison; August 23, 1984
Edison; August 23, 1984
        Inspection of Davis-Besse Reactor Coolant Pumps 2-1 and 2-2, Flowserve to First
Inspection of Davis-Besse Reactor Coolant Pumps 2-1 and 2-2, Flowserve to First
        Energy; September 16, 2002
Energy; September 16, 2002
        Issuance of Amendment 11 to Facility Operating License NPF-3 for Davis-Besse
Issuance of Amendment 11 to Facility Operating License NPF-3 for Davis-Besse
        Nuclear Power Station Unit 1, NRC to Toledo Edison; June 16, 1978
Nuclear Power Station Unit 1, NRC to Toledo Edison; June 16, 1978
        Reactor Coolant Pump Inter-Gasket Leakoff, Flowserve to First Energy; July 2, 2002
Reactor Coolant Pump Inter-Gasket Leakoff, Flowserve to First Energy; July 2, 2002
        Return to Service of Davis-Besse Reactor Coolant Pumps 2-1 and 2-2, Flowserve to
Return to Service of Davis-Besse Reactor Coolant Pumps 2-1 and 2-2, Flowserve to
        First Energy; February 4, 2003
First Energy; February 4, 2003
                                              A31                                  Attachment


Attachment
A32
Licensee Event Reports (LERs)
Licensee Event Reports (LERs)
      LER 2002-006; EDG Exhaust Piping Not Adequately Protected From Potential Tornado-
LER 2002-006; EDG Exhaust Piping Not Adequately Protected From Potential Tornado-
      Generated Missiles; November 5, 2002
Generated Missiles; November 5, 2002
      LER-2002-008; Review and Evaluate Containment Air Coolers Collective Significance
LER-2002-008; Review and Evaluate Containment Air Coolers Collective Significance
      LER; Revisions 0 and 1
LER; Revisions 0 and 1
      LER-2002-009; Degradation of High Pressure Injection Thermal Sleeves;
LER-2002-009; Degradation of High Pressure Injection Thermal Sleeves;
      February 3, 2002
February 3, 2002
      LER 2003-007; AC System Analysis Shows Potential Loss of Off-Site Power Following
LER 2003-007; AC System Analysis Shows Potential Loss of Off-Site Power Following
      Design Basis Event; August 5, 2003
Design Basis Event; August 5, 2003
Maintenance Work Orders
Maintenance Work Orders
      1-87-3304-00; Check Stud Elongation on All Four Reactor Coolant Pumps;
1-87-3304-00; Check Stud Elongation on All Four Reactor Coolant Pumps;
      July 21, 1988
July 21, 1988
      1-97-0553-00; Check P36-1 Casing Studs; May 14, 1998
1-97-0553-00; Check P36-1 Casing Studs; May 14, 1998
      1-97-0553-01; Check P36-2 Casing Studs; May 14, 1998
1-97-0553-01; Check P36-2 Casing Studs; May 14, 1998
      1-97-0553-02; Check P36-3 Casing Studs; May 14, 1998
1-97-0553-02; Check P36-3 Casing Studs; May 14, 1998
      1-97-0553-03; Check P36-4 Casing Studs; May 14, 1998
1-97-0553-03; Check P36-4 Casing Studs; May 14, 1998
      1-97-0817-04; Reactor Coolant Pump Motor 2-2; April 15, 1998
1-97-0817-04; Reactor Coolant Pump Motor 2-2; April 15, 1998
      7-96-0650-01, -02, and -05; Enclosure 7 of DB-MM-09117, R0, Tensioning Data Sheet
7-96-0650-01, -02, and -05; Enclosure 7 of DB-MM-09117, R0, Tensioning Data Sheet
      from Work Orders for Reactor Coolant Pumps 1-1, 1-2, and 2-1, Respectively
from Work Orders for Reactor Coolant Pumps 1-1, 1-2, and 2-1, Respectively
      7-96-0650-06; Work in Progress Log, Reactor Coolant Pump 2-2
7-96-0650-06; Work in Progress Log, Reactor Coolant Pump 2-2
      02-002724-000; Replace Upper Shaft Labyrinth Seal on Reactor Coolant Pump 2-2;
02-002724-000; Replace Upper Shaft Labyrinth Seal on Reactor Coolant Pump 2-2;
      May 6, 2002
May 6, 2002
      02-007012-000; Service Water Pumps and Piping; March 7, 2003
02-007012-000; Service Water Pumps and Piping; March 7, 2003
      02-007451-000; Temperature Indicator at Service Water Header 1; March 5, 2003
02-007451-000; Temperature Indicator at Service Water Header 1; March 5, 2003
Miscellaneous Documents
Miscellaneous Documents
      Basic Cause Categories Chart; February 27, 1996
Basic Cause Categories Chart; February 27, 1996
      Component Parameter Scoping Sheet for Reactor Coolant Pump Vibration Monitoring
Component Parameter Scoping Sheet for Reactor Coolant Pump Vibration Monitoring
      1012; Revision 3
1012; Revision 3
      CNRB Loss Prevention Subcommittee Meeting; April 23, 2003
CNRB Loss Prevention Subcommittee Meeting; April 23, 2003
                                            A32                                  Attachment


Attachment
A33
Condition Report Trending Presentation; August 13, 2003
Condition Report Trending Presentation; August 13, 2003
Corrective Action Program Performance Indicators; various dates
Corrective Action Program Performance Indicators; various dates
Line 6,440: Line 7,174:
July 28, 1999
July 28, 1999
License Amendment Request 03-0002; to Revise TS 3/4.5.2 ECCS Subsystems - Tavg
License Amendment Request 03-0002; to Revise TS 3/4.5.2 ECCS Subsystems - Tavg
> 280EF; Revision 25
> 280F; Revision 25
Managers Communication and Teamwork Meeting; August 26 and 28, 2003
Managers Communication and Teamwork Meeting; August 26 and 28, 2003
NEI 96-07; Guidelines for 10 CFR 50.59 Implementation; Revision 1
NEI 96-07; Guidelines for 10 CFR 50.59 Implementation; Revision 1
Line 6,457: Line 7,191:
Restart Performance Indicators; August 3, 2003
Restart Performance Indicators; August 3, 2003
Taproot Root Cause Tree Chart; February 27, 1996
Taproot Root Cause Tree Chart; February 27, 1996
                                      A33                                  Attachment


      Technical Specification Table 3.3-4
Attachment
      Three Day CA Look Ahead; March, 19, 2003
A34
      Time Line for Reactor Coolant Pump Casing Stud Tension Evaluation; August 15,2003
Technical Specification Table 3.3-4
      USAR Change 02-063; Revise Safety Analysis Report to Reflect Use of TORMIS;
Three Day CA Look Ahead; March, 19, 2003
      November 22, 2002
Time Line for Reactor Coolant Pump Casing Stud Tension Evaluation; August 15,2003
      USAR Chapter 8; Electrical
USAR Change 02-063; Revise Safety Analysis Report to Reflect Use of TORMIS;
      USAR Figure 9.3-16; Functional Drawing Makeup and Purification System; Revision 20
November 22, 2002
USAR Chapter 8; Electrical
USAR Figure 9.3-16; Functional Drawing Makeup and Purification System; Revision 20
NQA Audits and Self Assessment Reports
NQA Audits and Self Assessment Reports
      DB-C-02-02; NQA Assessment Report; August 9, 2002
DB-C-02-02; NQA Assessment Report; August 9, 2002
      DB-C-02-03; NQA Assessment Report; November 14, 2002
DB-C-02-03; NQA Assessment Report; November 14, 2002
      DB-C-02-04; NQA Assessment Report; February 19, 2003
DB-C-02-04; NQA Assessment Report; February 19, 2003
      DB-C-03-01; NQA Assessment Report; May 28, 2003
DB-C-03-01; NQA Assessment Report; May 28, 2003
      DB-C-03-02; NQA Assessment Report; September 1, 2003
DB-C-03-02; NQA Assessment Report; September 1, 2003
      DB-C-03-03; NQA Assessment Report; November 17, 2003
DB-C-03-03; NQA Assessment Report; November 17, 2003
      2002-0085; Self Assessment Report, Operating Experience Program; October 3, 2002
2002-0085; Self Assessment Report, Operating Experience Program; October 3, 2002
      Self Evaluation Report; June 2002
Self Evaluation Report; June 2002
      Self Assessment Report, Electrical Transient Analysis Program (ETAP) June 2-6, 2003;
Self Assessment Report, Electrical Transient Analysis Program (ETAP) June 2-6, 2003;
      Revision 1
Revision 1
NUREGs
NUREGs
      0800; Standard Review Plan for the Review of Safety Analysis Reports for Nuclear
0800; Standard Review Plan for the Review of Safety Analysis Reports for Nuclear
      Power Plants; Revision 1
Power Plants; Revision 1
      1649; Reactor Oversight Process; Revision 3; July 2000
1649; Reactor Oversight Process; Revision 3; July 2000
      CR 6762; GSI-191 Technical Assessment: Parametric Evaluations for Pressurized
CR 6762; GSI-191 Technical Assessment: Parametric Evaluations for Pressurized
      Water Reactor Recirculation Sump Performance; August 2002
Water Reactor Recirculation Sump Performance; August 2002
Potential Condition Adverse to Quality Reports
Potential Condition Adverse to Quality Reports
      1991-0173; ECCS Room Cooling Units; May 14, 1991
1991-0173; ECCS Room Cooling Units; May 14, 1991
      1993-0256; Potential Condition Adverse to Quality Report; April 19, 1993
1993-0256; Potential Condition Adverse to Quality Report; April 19, 1993
                                            A34                                  Attachment


      1998-0126; Post Accident Sampling Pump P-218 Has Seal Design Which Is Not Leak
Attachment
      Tight; January 25, 1998
A35
1998-0126; Post Accident Sampling Pump P-218 Has Seal Design Which Is Not Leak
Tight; January 25, 1998
Procedures
Procedures
      Self Evaluation Process Guidelines; April 25, 2001
Self Evaluation Process Guidelines; April 25, 2001
      DBBP-LP-2000; Condition Report Process Implementation Expectations; April 4, 2003
DBBP-LP-2000; Condition Report Process Implementation Expectations; April 4, 2003
      DBBP-PI-2005; Cause Analysis Review Group; February 7, 2003
DBBP-PI-2005; Cause Analysis Review Group; February 7, 2003
      DB-ME-03002; Station Battery Service and Performance Discharge Test; Revision 4
DB-ME-03002; Station Battery Service and Performance Discharge Test; Revision 4
      DB-ME-09500; Installation and Termination of Electrical Cables
DB-ME-09500; Installation and Termination of Electrical Cables
      DB-MM-09320; Jacket Water Heat Exchanger Maintenance; Revision 5
DB-MM-09320; Jacket Water Heat Exchanger Maintenance; Revision 5
      DB-OP-01200; Reactor Coolant System Leakage Management; Revision 5
DB-OP-01200; Reactor Coolant System Leakage Management; Revision 5
      DB-OP-02037; Emergency Diesel Generator Alarm Panel 37 Operating Procedure;
DB-OP-02037; Emergency Diesel Generator Alarm Panel 37 Operating Procedure;
      Revision 2
Revision 2
      DB-OP-06016; Containment Air Cooler System Operating Procedure; Revision 2
DB-OP-06016; Containment Air Cooler System Operating Procedure; Revision 2
      DB-OP-06261; Service Water System Operating Procedure; Revision 2
DB-OP-06261; Service Water System Operating Procedure; Revision 2
      DB-OP-06406; Steam and Feedwater Rupture Control System Operation Procedure;
DB-OP-06406; Steam and Feedwater Rupture Control System Operation Procedure;
      Revision 4
Revision 4
      DB-PF-03008; Containment Local Leakage Rate Tests; Revision 5
DB-PF-03008; Containment Local Leakage Rate Tests; Revision 5
      DB-PF-03020; Service Water Train 1 Valve Test; Revision 5
DB-PF-03020; Service Water Train 1 Valve Test; Revision 5
      DB-PF-03027; Service Water Train 2 Valve Test; Revision 5
DB-PF-03027; Service Water Train 2 Valve Test; Revision 5
      DB-PF-03117; Baseline and Comprehensive Testing of Service Water Pump 1;
DB-PF-03117; Baseline and Comprehensive Testing of Service Water Pump 1;
      Revision 3
Revision 3
      DB-PF-03123; Baseline and Comprehensive Testing of Service Water Pump 2;
DB-PF-03123; Baseline and Comprehensive Testing of Service Water Pump 2;
      Revision 5
Revision 5
      DB-PF-03130; Baseline and Comprehensive Testing of Service Water Pump 3;
DB-PF-03130; Baseline and Comprehensive Testing of Service Water Pump 3;
      Revision 5
Revision 5
      DB-PF-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed
DB-PF-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed
      Trip Test; Revision 5
Trip Test; Revision 5
      DB-SC-03023; Off-site AC Sources Lined Up and Available; Revision 6
DB-SC-03023; Off-site AC Sources Lined Up and Available; Revision 6
                                            A35                              Attachment


      DB-SP-03000; Service Water Integrated Train I Flow Balance Procedure
Attachment
      DB-SP-03001; Service Water Integrated Train II Flow Balance Procedure
A36
      DB-SP-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed
DB-SP-03000; Service Water Integrated Train I Flow Balance Procedure
      Trip Test
DB-SP-03001; Service Water Integrated Train II Flow Balance Procedure
      EN-DP-01080; Calculations; Revision 0
DB-SP-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed
      NG-EN-00327; RCS Integrated Leakage Program; Revision 0
Trip Test
      NG-EN-00385; Program Compliance Review; Revision 0
EN-DP-01080; Calculations; Revision 0
      NG-NA-00711; Quality Trending; March 1, 2003
NG-EN-00327; RCS Integrated Leakage Program; Revision 0
      NG-VP-00100; Restart Action Plan Process; February 6, 2003
NG-EN-00385; Program Compliance Review; Revision 0
      NOBP-LP-2007; Condition Report Process Effectiveness Review; March 1, 2003
NG-NA-00711; Quality Trending; March 1, 2003
      NOBP-LP-2001; FENOC Focus Self Assessment Guideline; Revisions 0 and 1
NG-VP-00100; Restart Action Plan Process; February 6, 2003
      NOBP-LP-2004; FENOC Ongoing Self Assessment Guideline; Revision 0
NOBP-LP-2007; Condition Report Process Effectiveness Review; March 1, 2003
      NOBP-LP-2008; Corrective Action Review Board; Revision 0
NOBP-LP-2001; FENOC Focus Self Assessment Guideline; Revisions 0 and 1
      NOBP-LP-2010; Crest Trending Codes; Revision 0
NOBP-LP-2004; FENOC Ongoing Self Assessment Guideline; Revision 0
      NOP-CC-3002; Nuclear Operating Administrative Procedure; Revision 0
NOBP-LP-2008; Corrective Action Review Board; Revision 0
      NOP-ER-1001; Continuous Equipment Performance Improvement; Revision 1
NOBP-LP-2010; Crest Trending Codes; Revision 0
      NOP-ER-3001; Problem Solving and Decision Making Process; Revision 0
NOP-CC-3002; Nuclear Operating Administrative Procedure; Revision 0
      NOP-LP-2001; Condition Report Process; Revisions 3 and 4
NOP-ER-1001; Continuous Equipment Performance Improvement; Revision 1
      NOP-LP-2004; Internal Assessment Process; Revision 1
NOP-ER-3001; Problem Solving and Decision Making Process; Revision 0
      RA-EP-02830; Emergency Plan Off Normal Occurrence Procedure; Revision 1
NOP-LP-2001; Condition Report Process; Revisions 3 and 4
NOP-LP-2004; Internal Assessment Process; Revision 1
RA-EP-02830; Emergency Plan Off Normal Occurrence Procedure; Revision 1
Regulatory Guides
Regulatory Guides
      1.4; Assumptions Used for Evaluating the Potential Radiological Consequences of a
1.4; Assumptions Used for Evaluating the Potential Radiological Consequences of a
      Loss of Coolant Accident for Pressurized Water Reactors; Revision 2
Loss of Coolant Accident for Pressurized Water Reactors; Revision 2
      1.187; Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and
1.187; Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and
      Experiments; November 2000.
Experiments; November 2000.
                                            A36                                Attachment


Attachment
A37
Reports
Reports
        Corrective Action Program Review Summary Report; September 2002
Corrective Action Program Review Summary Report; September 2002
        Collective Significance Report Containment Air Cooler Thermal Performance;
Collective Significance Report Containment Air Cooler Thermal Performance;
        March 21, 2003
March 21, 2003
        Assessment of Thermal Performance for the Containment Air Coolers; April 22, 2003
Assessment of Thermal Performance for the Containment Air Coolers; April 22, 2003
        Assessment of Thermal Performance for the Containment Air Coolers; August 9, 2003
Assessment of Thermal Performance for the Containment Air Coolers; August 9, 2003
        Emergency Diesel Generator 1 Jacket Water Cooler Eddy Current Test Report;
Emergency Diesel Generator 1 Jacket Water Cooler Eddy Current Test Report;
        July 31, 2002
July 31, 2002
        Emergency Diesel Generator 2 Jacket Water Cooler Eddy Current Test Report;
Emergency Diesel Generator 2 Jacket Water Cooler Eddy Current Test Report;
        July 9, 2003
July 9, 2003
        Operating Experience Report 15262; Byron Jackson Reactor Coolant Pump
Operating Experience Report 15262; Byron Jackson Reactor Coolant Pump
        Casing-to-cover Leakage; January 23, 2003
Casing-to-cover Leakage; January 23, 2003
        Operating Experience Report 15383; Preliminary Linear Indications on the Reactor
Operating Experience Report 15383; Preliminary Linear Indications on the Reactor
        Coolant Pump 1-1 Shaft Assembly; January 21, 2003
Coolant Pump 1-1 Shaft Assembly; January 21, 2003
Surveillances
Surveillances
        DB-ME-03002; Battery Service Test; completed March 2002
DB-ME-03002; Battery Service Test; completed March 2002
        DB-PF-03065; Pressure and Augmented Leakage Test; completed April 2, 2000,
DB-PF-03065; Pressure and Augmented Leakage Test; completed April 2, 2000,
        August 27, 2002, and August 28, 2002
August 27, 2002, and August 28, 2002
        DB-PF-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed
DB-PF-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed
        Trip Test; completed May 10, 2002
Trip Test; completed May 10, 2002
        DB-SP-03357; Reactor Coolant System Water Inventory Balance; completed
DB-SP-03357; Reactor Coolant System Water Inventory Balance; completed
        May 3, 1993, November 21, 1994, May 29, 1996, May 23, 1998, and May 22, 2000
May 3, 1993, November 21, 1994, May 29, 1996, May 23, 1998, and May 22, 2000
        DB-SP-03358; Reactor Coolant System Flow Rate Test; completed August 25, 2000
DB-SP-03358; Reactor Coolant System Flow Rate Test; completed August 25, 2000
        DB-SP-04360; Reactor Coolant System Flow Test; completed August 11, 2000
DB-SP-04360; Reactor Coolant System Flow Test; completed August 11, 2000
        DB-SP-04363; Reactor Coolant Pumps Hand Rotation; completed August 19, 2003,
DB-SP-04363; Reactor Coolant Pumps Hand Rotation; completed August 19, 2003,
        September 23, 2003, and October 23, 2003
September 23, 2003, and October 23, 2003
10 CFR 50.59 Applicability Determination, Screen and Evaluations
10 CFR 50.59 Applicability Determination, Screen and Evaluations
        02-01740; TORMIS Methodology for Tornado Missile Risk Evaluation;
02-01740; TORMIS Methodology for Tornado Missile Risk Evaluation;
        November 13, 2002
November 13, 2002
                                              A37                                  Attachment


      03-00087; Screen Use of Fuel Assemblies with Spacer Grid Damage in the Cycle 14
Attachment
      Core - Modes 3, 4, 5, 6; February 1, 2003
A38
03-00087; Screen Use of Fuel Assemblies with Spacer Grid Damage in the Cycle 14
Core - Modes 3, 4, 5, 6; February 1, 2003
Vendor Manual
Vendor Manual
      03-5001383-01; Reactor Coolant Pump Motor Bearing Maintenance, Pages 89AA
03-5001383-01; Reactor Coolant Pump Motor Bearing Maintenance, Pages 89AA
      through 105; completed April 17 through May 6, 1998
through 105; completed April 17 through May 6, 1998
      M-001-1; Westinghouse Product Update: Recommended 1-Year, 5-Year, and 10-Year
M-001-1; Westinghouse Product Update: Recommended 1-Year, 5-Year, and 10-Year
      Reactor Coolant Pump Motor Inspection and Maintenance; November 1991
Reactor Coolant Pump Motor Inspection and Maintenance; November 1991
                                            A38                              Attachment


                          LIST OF ACRONYMS USED
Attachment
AC     Alternating Current
A39
ADAMS Agency-wide Document Access and Management System
LIST OF ACRONYMS USED
AIT   Augmented Inspection Team
AC
AFW   Auxiliary Feedwater
Alternating Current
ASME   American Society of Mechanical Engineers
ADAMS
AV     Apparent Violation
Agency-wide Document Access and Management System
BACC   Boric Acid Corrosion Control
AIT
BWST   Borated Water Storage Tank
Augmented Inspection Team
B&W   Babcock and Wilcox
AFW
CAC   Containment Air Cooler
Auxiliary Feedwater
CARB   Corrective Action Review Board
ASME
CAP   Corrective Action Program
American Society of Mechanical Engineers
CATI   Corrective Action Team Inspection
AV
CCW   Component Cooling Water
Apparent Violation
CFR   Code of Federal Regulations
BACC
CR     Condition Report
Boric Acid Corrosion Control
CRDM   Control Rod Drive Mechanism
BWST
CS     Containment Spray
Borated Water Storage Tank
DC     Direct Current
B&W
DHR   Decay Heat Removal
Babcock and Wilcox
EAB   Engineering Assessment Board
CAC
ECCS   Emergency Core Cooling System
Containment Air Cooler
ECR   Engineering Change Request
CARB
EDG   Emergency Diesel Generator
Corrective Action Review Board
EPRI   Electric Power Research Institute
CAP
EQ     Environmental Qualification
Corrective Action Program
ESF   Engineered Safety Feature
CATI
ETAP   Electric Transient Analysis Profile
Corrective Action Team Inspection
FENOC FirstEnergy Nuclear Operating Company
CCW
FIN   Finding
Component Cooling Water
GDC   General Design Criteria
CFR
GL     Generic Letter
Code of Federal Regulations
GPM   Gallons per Minute
CR
HPI   High Pressure Injection
Condition Report
HPR   High Pressure Recirculation
CRDM
IMC   Inspection Manual Chapter
Control Rod Drive Mechanism
IN     Information Notice
CS
IR     Inspection Report
Containment Spray
ISI   In-service Inspection
DC
IST   In-service Testing
Direct Current
KSI   Kilo (1000) Pounds per Square Inch
DHR
kV     Kilo Volt (1000 volts)
Decay Heat Removal
LAR   License Amendment Request
EAB
lb/ft3 Pounds per Cubic Foot
Engineering Assessment Board
LER   Licensee Event Report
ECCS
LIR   Latent Issues Review
Emergency Core Cooling System
LOCA   Loss of Coolant Accident
ECR
                                      A39              Attachment
Engineering Change Request
EDG
Emergency Diesel Generator
EPRI
Electric Power Research Institute
EQ
Environmental Qualification
ESF
Engineered Safety Feature
ETAP
Electric Transient Analysis Profile
FENOC
FirstEnergy Nuclear Operating Company
FIN
Finding
GDC
General Design Criteria
GL
Generic Letter
GPM
Gallons per Minute
HPI
High Pressure Injection
HPR
High Pressure Recirculation
IMC
Inspection Manual Chapter
IN
Information Notice
IR
Inspection Report
ISI
In-service Inspection
IST
In-service Testing
KSI
Kilo (1000) Pounds per Square Inch
kV
Kilo Volt (1000 volts)
LAR
License Amendment Request
lb/ft3
Pounds per Cubic Foot
LER
Licensee Event Report
LIR
Latent Issues Review
LOCA
Loss of Coolant Accident


                        LIST OF ACRONYMS USED, contd.
Attachment
LOOP     Loss of Offsite Power
A40
LPI     Low Pressure Injection
LIST OF ACRONYMS USED, contd.
MRB     Management Review Board
LOOP
MSSV     Main Steam Safety Valve
Loss of Offsite Power
NCV     Non-Cited Violation
LPI
NEI     Nuclear Energy Institute
Low Pressure Injection
NOBP     Nuclear Operations Business Practice
MRB
NOP/NOT Normal Operating Pressure and Normal Operating Temperature
Management Review Board
NPSH     Net Positive Suction Head
MSSV
NQA     Nuclear Quality Assessment
Main Steam Safety Valve
NRC     United States Nuclear Regulatory Commission
NCV
NRR     Office of Nuclear Reactor Regulation
Non-Cited Violation
OI       Office of Investigations
NEI
PARS     Publicly Available Records
Nuclear Energy Institute
PI       Performance Indicator
NOBP
PORV     Power Operated Relief Valve
Nuclear Operations Business Practice
PRA     Probabilistic Risk Assessment
NOP/NOT
PRC     Project Review Committee
Normal Operating Pressure and Normal Operating Temperature
PSIG     Pounds Per Square Inch Gauge
NPSH
RCPB     Reactor Coolant Pressure Boundary
Net Positive Suction Head
RCP     Reactor Coolant Pump
NQA
RCS     Reactor Coolant System
Nuclear Quality Assessment
RFO     Refueling Outage
NRC
RSRB     Restart Station Review Board
United States Nuclear Regulatory Commission
SCAQ     Significant Condition Adverse to Quality
NRR
SDP     Significance Determination Process
Office of Nuclear Reactor Regulation
SG       Steam Generator
OI
SHA     System Health Assurance
Office of Investigations
SRA     Senior Reactor Analyst
PARS
SRB     Station Review Board
Publicly Available Records
SSC     Structures, Systems, Components
PI
SSDI     Safety System Design and Performance Capability Inspection
Performance Indicator
SW       Service Water
PORV
the Code ASME Boiler and Nuclear Pressure Vessel Code
Power Operated Relief Valve
TPCS     Transient without Power Conversion System
PRA
TS       Technical Specifications
Probabilistic Risk Assessment
TSP     Tri-Sodium Phosphate
PRC
UHS     Ultimate Heat Sink
Project Review Committee
URI     Unresolved Item
PSIG
USAR     Updated Safety Analysis Report
Pounds Per Square Inch Gauge
V       Volts
RCPB
Vac     Volts (alternating current)
Reactor Coolant Pressure Boundary
Vdc     Volts (direct current)
RCP
VIO     Violation
Reactor Coolant Pump
WO       Work Order
RCS
EF      Degrees Fahrenheit
Reactor Coolant System
                                        A40                        Attachment
RFO
Refueling Outage
RSRB
Restart Station Review Board
SCAQ
Significant Condition Adverse to Quality
SDP
Significance Determination Process
SG
Steam Generator
SHA
System Health Assurance
SRA
Senior Reactor Analyst
SRB
Station Review Board
SSC
Structures, Systems, Components
SSDI
Safety System Design and Performance Capability Inspection
SW
Service Water
the Code
ASME Boiler and Nuclear Pressure Vessel Code
TPCS
Transient without Power Conversion System
TS
Technical Specifications
TSP
Tri-Sodium Phosphate
UHS
Ultimate Heat Sink
URI
Unresolved Item
USAR
Updated Safety Analysis Report
V
Volts
Vac  
Volts (alternating current)
Vdc  
Volts (direct current)
VIO
Violation
WO
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Latest revision as of 04:32, 16 January 2025

IR 05000346-03-010(DRS); 03/17/2003 - 01/07/2004; Davis-Besse Nucler Power Station; Corrective Action Program Implementation Effectiveness
ML040680070
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 03/05/2004
From: Grobe J
NRC/RGN-III
To: Myers L
FirstEnergy Nuclear Operating Co
References
EA-04-049, EA-04-050, FOIA/PA-2004-0277 IR-03-010
Download: ML040680070 (172)


See also: IR 05000346/2003010

Text

March 5, 2004

EA-04-049

EA-04-050

Mr. Lew W. Myers

Chief Operating Officer

FirstEnergy Nuclear Operating Company

Davis-Besse Nuclear Power Station

5501 North State Route 2

Oak Harbor, OH 43449-9760

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION

NRC SPECIAL TEAM INSPECTION - CORRECTIVE ACTION PROGRAM

IMPLEMENTATION - REPORT 05000346/2003010(DRS) AND NOTICE of

VIOLATION

Dear Mr. Myers:

On January 7, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed a special

corrective action team inspection (CATI) at your Davis-Besse Nuclear Power Station to assess

the effectiveness of the implementation of your corrective action program. This inspection

represented a significant input into the NRCs Davis-Besse Oversight Panels (Panel) review of

Restart Checklist Item 3.a, "Corrective Action Program and also contributed to the Panels

review of Restart Checklist Items No. 2.c, "Structures, Systems, and Components Inside

Containment," and 5.b, "Systems Readiness for Restart." The enclosed inspection report

documents the CATI findings which were discussed with you and other members of your staff on

September 9 and November 10, 2003, and on January 7, 2004.

The CATI was accomplished by eleven NRC inspectors and contractors over a period of ten

months involving five weeks of onsite effort and multiple additional weeks of in-office review.

The CATI evaluated the effectiveness of the implementation of various aspects of your

corrective action program (CAP), including: (1) identifying and documenting plant design-related

deficiencies; (2) categorizing and prioritizing safety issues for resolution; (3) conducting

apparent and root cause analyses; (4) determining extent of condition and (5) implementing

appropriate and timely corrective actions to ensure adequate resolution of problems. Overall,

the CATI team reviewed the resolution of several hundred conditions adverse to quality. Many

of the deficiencies reviewed by the CATI involved safety system design engineering issues.

In addition, the CATI reviewed management involvement in and oversight of the implementation

of the corrective action program, including the routine performance indicators utilized to monitor

the program implementation, and the effectiveness of conditions adverse to quality trending

analyses and quality assessment audits of the CAP implementation. Finally, due to the nature

of multiple NRC inspection findings, the team focused additional effort on assessing the

adequacy of engineering work products, including analyses and calculations.

Notwithstanding a significant number of performance deficiencies identified during the

inspection, based on input from the CATI team, the Panel concluded that the corrective action

program was sufficiently acceptable for plant restart. The significance of each performance

L. Myers

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deficiency identified during the inspection was evaluated in accordance with the NRCs

Significance Determination Process and concluded to be of very low safety significance. While

the individual risk significance of each performance deficiency was low, two themes emerged

from a collective evaluation of the number and nature of the CATI findings:



A weakness in identifying and evaluating the nature and extent of issues when

performing apparent cause evaluations to identify the cause(s) and full scope of

necessary corrective actions, particularly in the area of safety system design

deficiencies; and



A weakness in the quality of engineering work products, including design calculations

and analyses, to correct conditions adverse to quality.

In addition, the CATI noted that during early part of the extended shutdown of the Davis-Besse

facility, you suspended the conditions adverse to quality trending program intended to provide

early identification of broader plant equipment and organizational concerns. Your resumption of

the trending program was not timely. Further, your corrective action program required the

review of the effectiveness of corrective action taken to address significant conditions adverse

to quality six months after implementation of those actions. Sufficient actions had not been

completed for six months for the CATI to evaluate this area.

Following the conclusion of the onsite phase of the inspection in September 2003, your staff

implemented actions to further assess the specific areas identified by the CATI and develop

improvement initiatives to address those areas. Those activities were presented publicly to the

NRC on November 12, 2003 and discussed further during a public meeting on December 10,

2003. Continuing actions to further address the areas of corrective action program

effectiveness and engineering product quality are documented in your Operational

Improvement Plan, Operating Cycle 14, Revision 3, submitted on February 19, 2003.

The CATI team has reviewed these ongoing and planned actions and concluded that, if

properly implemented, they should address the concerns identified during this inspection and

further improve the corrective action program effectiveness at Davis-Besse. However, the

effectiveness of the actions could not be evaluated by the NRC at this time due to the relatively

short implementation time of many of those corrective actions.

The team noted that, in general, the Nuclear Quality Assurance (NQA) assessments of

corrective action program effectiveness identified problems pertaining to corrective action

program implementation that were similar to the issues identified by the CATI. However,

resolution of NQAs findings was not sufficiently prompt or effective to address the identified

problems and to prevent the underlying deficiencies that led to these NRC findings. Continuing

diligence by Davis-Besse management will be necessary to assure lasting effective corrective

action program implementation. The NRC will continue to closely monitor Davis-Besses

performance to assess the effectiveness of the Davis-Besse corrective actions.

In addition to documenting the results of the CATI, this inspection report documents the closure

of Davis-Besse Restart Checklist Items 2.c, "Structures, Systems, and Components Inside

L. Myers

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Containment," and 3.a, "Corrective Action Program." Restart checklist item 5.b, Systems

Readiness for Restart, is not closed in this inspection report.

Based on the results of this inspection, the NRC identified two violations which are cited in the

enclosed Notice of Violation (Notice) and the circumstances surrounding them are described in

detail in the subject inspection report. The violations are being cited because your staff failed to

restore compliance after the violations were identified.

Additionally, the NRC identified twenty-six NRC-identified violations of very low safety

significance (Green) and one NRC-identified Severity Level IV violation. These violations are

being treated as Non-Cited Violations (NCVs) consistent with Section VI.A of the Enforcement

Policy. These NCVs are described in the subject inspection report. The violations were

evaluated in accordance with the "General Statement of Policy and Procedure for NRC

Enforcement Actions," (Enforcement Policy), NUREG -1600. The current Enforcement Policy is

included on the NRCs web site at www.nrc.gov; select What we do, Enforcement, then

Enforcement Policy.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. The NRC will use your response, in part, to

determine whether further enforcement action is necessary to ensure compliance with

regulatory requirements.

If you contest the severity level or significance of the NCVs described in the report, you should

also provide a response within 30 days of the date of this inspection report, with the basis for

your denial, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001, with copies to the Regional Administrator, Region III, 801

Warrenville Road, Suite 255, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-001.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter

and its enclosures will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRC's

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

L. Myers

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To the extent possible, your response should not include any personal privacy, proprietary, or

safeguards information so that it can be made available to the Public without redaction.

Sincerely,

/RA/

John A. Grobe, Chairman

Davis-Besse Oversight Panel

Docket No. 50-346

License No. NPF-3

Enclosures:

1. Notice of Violation

2. Inspection Report No. 05000346/2003010(DRS)

cc w/encl:

The Honorable Dennis Kucinich

G. Leidich, President - FENOC

Plant Manager

Manager - Regulatory Affairs

M. OReilly, Attorney, FirstEnergy

Ohio State Liaison Officer

R. Owen, Administrator, Ohio Department of Health

Public Utilities Commission of Ohio

President, Board of County Commissioners

Of Lucas County

Steve Arndt, President, Ottawa County Board of Commissioners

D. Lochbaum, Union Of Concerned Scientists

J. Riccio, Greenpeace

P. Gunter, N.I.R.S.

L. Myers

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To the extent possible, your response should not include any personal privacy, proprietary, or

safeguards information so that it can be made available to the Public without redaction.

Sincerely,

/RA/

John A. Grobe, Chairman

Davis-Besse Oversight Panel

Docket No. 50-346

License No. NPF-3

Enclosures:

1. Notice of Violation

2. Inspection Report No. 05000346/2003010(DRS)

cc w/encl:

The Honorable Dennis Kucinich

G. Leidich, President - FENOC

Plant Manager

Manager - Regulatory Affairs

M. OReilly, Attorney, FirstEnergy

Ohio State Liaison Officer

R. Owen, Administrator, Ohio Department of Health

Public Utilities Commission of Ohio

President, Board of County Commissioners

Of Lucas County

Steve Arndt, President, Ottawa County Board of Commissioners

D. Lochbaum, Union Of Concerned Scientists

J. Riccio, Greenpeace

P. Gunter, N.I.R.S.

DOCUMENT NAME: C:\\ORPCheckout\\FileNET\\ML040680070.WPD

To receive a copy of this document, indicate in the box: "C" = Copy without enclosure "E"= Copy with enclosure "N"= No copy

OFFICE

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NAME

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DATE

03/05/04

did not concur

03/05/04

03/05/04

OFFICE

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NAME

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JGrobe

DATE

03/05/04

03/05/04

OFFICIAL RECORD COPY

L. Myers

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ADAMS Distribution:

AJM

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C. Ariano (hard copy)

C. Pederson, DRS (hard copy - IRs only)

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Notice of Violation

-1-

NOTICE OF VIOLATION

First Energy Nuclear Operating Company

Docket No. 50-346

Davis-Besse Nuclear Power Station

License No. NPF-3

EA-04-049

EA-04-050

During an NRC inspection conducted from March 17, 2003 through January 7, 2004, violations

of NRC requirements was identified. In accordance with the "General Statement of Policy and

Procedure for NRC Enforcement Actions," NUREG-1600, the violations are listed below:

(a)

Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that measures be

established to assure that applicable regulatory requirements and the design basis are

correctly translated into specifications, drawings, procedures, and instructions. It also

requires that measures be provided for verifying or checking the adequacy of design,

such as by the performance of design reviews, by the use of alternate or simplified

calculational methods, or by the performance of a suitable testing program.

Contrary to the above, as of August 12, 2003, the licensee failed to verify that the

design of the service water system discharge path swapover setpoints was adequate.

Specifically, the analysis performed by the licensee showed that the established

setpoints were not adequate and the evaluation of the analysis accepted the inadequate

setpoint based on non-safety-related equipment performing a safety-related function

under design basis conditions. Neither the analysis nor the evaluation corrected the

nonconforming condition previously identified in Inspection Report 05000346/2002014.

This is a violation of very low safety significance (Green).

(b)

Technical Specification Section 4.05a requires, in part, that the licensee perform

inservice testing of valves in accordance with the ASME OM Code and applicable

addenda as required by 10 CFR 50.55a.

10 CFR 50.55a(f)(4) requires that pumps and valves which are classified as ASME

Code Class 1, 2, and 3 meet the inservice test requirements set forth in the appropriate

edition and addenda of the ASME OM Code. It further requires that, during 120-month

intervals successive to the initial 120-month interval, tests must comply with the

requirements in the latest Code edition and addenda incorporated by reference in

paragraph (b) of 10 CFR 50.55a 12 months prior to the start of the 120-month interval.

Paragraph 50.55a(f)(5)(i) requires that the inservice test program be revised as

necessary to meet the requirement of paragraph 50.55a(f)(4).

The ASME OM Code, 1995 edition through the 1996 addenda, Section ISTC 4.5.1

requires, in part, that check valves be exercised nominally every three months. Section

ISTC 4.5.4(a) requires, in part, that check valves be exercised by initiating flow and

observing that the obturator traveled to its full open position. Observations shall be

made by observing a direct indicator (e.g., a position-indicating device) or by other

Notice of Violation

-2-

positive means (e.g., changes in system pressure, flow rate, level, temperature, seat

leakage, testing, or non-intrusive testing results).

Contrary to the above, the NRC identified that on September 12, 2003, and other dates,

the licensee did not observe by a direct indicator or other positive means that the ASME

Class 3 service water pump discharge check valve obturator traveled to its full open

position during its quarterly surveillance test. Specifically, on September 12, 2003, the

licensee observed a flow rate of 9718 gpm through valve SW-19, which was less than

the test acceptance criterion of 10,000 gpm, and less than the approximately 10,300

gpm used in the licensees most recent accident analysis. Observing flow rates less

than required for the valve to perform its safety function was not a positive means to

determine that the obturator traveled to its full open position and no other direct indicator

or positive means was used. The NRC approved use of the 1995 Code edition through

the 1996 addenda for the third inservice testing 120-month interval on March 28, 2003 .

Prior to that date, the licensee was committed to the 1986 Edition (no Addenda) of the

ASME Boiler and Pressure Vessel Code,Section XI. The 1986 Code Edition contains

similar requirements.

This is a violation of very low safety significance (Green).

Pursuant to the provisions of 10 CFR 2.201, FirstEnergy Nuclear Operating Company is hereby

required to submit a written statement or explanation to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555 with a copy to the

Regional Administrator, Region III, and a copy to the NRC Resident Inspector at the

Davis-Besse Nuclear Power Plant, within 30 days of the date of the letter transmitting this

Notice of Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of

Violation; EA-04-049 and EA-04-050," and should include for each violation: (1) the reason for

the violation, or, if contested, the basis for disputing the violation or severity level; (2) the

corrective steps that have been taken and the results achieved; (3) the corrective steps that will

be taken to avoid further violations; and (4) the date when full compliance will be achieved.

Your response may reference or include previous docketed correspondence, if the

correspondence adequately addresses the required response. If an adequate reply is not

received within the time specified in this Notice, an order or a Demand for Information may be

issued as to why the license should not be modified, suspended, or revoked, or why such other

action as may be proper should not be taken. Where good cause is shown, consideration will

be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with

the basis for your denial, to the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the NRCs document system (ADAMS), accessible from the

NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should

not include any personal privacy, proprietary, or safeguards information so that it can be made

available to the public without redaction. If personal privacy or proprietary information is

necessary to provide an acceptable response, then please provide a bracketed copy of your

Notice of Violation

-3-

response that identifies the information that should be protected and a redacted copy of your

response that deletes such information. If you request withholding of such material, you must

specifically identify the portions of your response that you seek to have withheld and provide in

detail the basis for your claim of withholding (e.g., explain why the disclosure of information will

create an unwarranted invasion of personal privacy or provide the information required by

10 CFR 2.390(b) to support a request for withholding confidential commercial or financial

information). If safeguards information is necessary to provide an acceptable response, please

provide the level of protection described in 10 CFR 73.21.

Dated this 5th day of March, 2004

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-346

License No:

NPF-3

Report No:

05000346/2003010

Licensee:

FirstEnergy Nuclear Operating Company

Facility:

Davis-Besse Nuclear Power Station

Location:

5501 North State Route 2

Oak Harbor, OH 43449

Dates:

March 17, 2003 through January 07, 2004

Inspection Team:

Z. Falevits, Lead Senior Reactor Engineering Inspector

M. Farber, Senior Reactor Engineering Inspector

P. Lougheed, Senior Reactor Engineering Inspector

A. Walker, Senior Reactor Engineering Inspector

D. Chyu, Reactor Engineering Inspector

R. Daley, Reactor Engineering Inspector

F. Baxter, Electrical Consultant

W. Bennett, Corrective Action Consultant

Dr. O. Mazzoni, Electrical Consultant

J. Panchison, Mechanical Consultant

W. Sherbin, Mechanical Consultant

Approved by:

Julio F. Lara, Chief

Electrical Engineering Branch

Division of Reactor Safety

Enclosure

TABLE of CONTENTS

Section

Page

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

Inspector-Identified and Self-Revealed Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

REPORT DETAILS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

4.

OTHER ACTIVITIES (OA) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

Background . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

(1)

Corrective Action Program Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

.1

Adequacy of Licensees Efforts to Identify and Document

Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

.2

Adequacy of Licensees Efforts to Categorize and Prioritize

Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

.3

Adequacy of Licensees Efforts to Evaluate Identified Conditions . . . . . 17

.4

Adequacy of Licensees Efforts to Correct Identified Problems

. . . . . . 19

.5

Review of Engineering Products and Corrective Actions . . . . . . . . . . . 20

.6

Adequacy of Licensees Efforts to Resolve Procedure Adherence

and Quality Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

(2)

Review of the Licensees Internal Assessment Activities . . . . . . . . . . . . . . . . . 21

.1

Trending, Self-Assessment, and Evaluation Program

Implementation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

.2

Corrective Action Program Performance Indicators . . . . . . . . . . . . . . . 23

.3

Nuclear Quality Assessment Audits and Self Assessments of

Corrective Action Program Implementation . . . . . . . . . . . . . . . . . . . . . 24

(3)

Management CAP Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

4OA3 Event Response Follow-up - Special Inspection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

(1)

Background . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

Davis-Besse CAP Compliance Review . . . . . . . . . . . . . . . . . . . . . . . . . 27

Assessment of the Corrective Action Program Compliance Review . . . 27

(2)

Detailed Team Review of Licensee Corrective Actions Implemented to

Address Electrical Issues Previously Identified by NRC or the Licensee . . . . . 28

.1

Undervoltage Time Delay Relay Setting Did Not Account For

Instrument Uncertainties . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

.2

Lack of 480 Vac Class 1E Motor Thermal Overload Protection . . . . . . 30

.3

Failure to Perform Direct Current Contactor Testing to Ensure

Minimum Voltage at Motor Operated Valves

. . . . . . . . . . . . . . . . . . . . 31

Enclosure

ii

.4

Failure to Verify Adequacy of Short Circuit Protection for Direct

Current Circuits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

.5

Lack of Calculations to Ensure Minimum Voltage Availability at

Device Terminals . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

.6

Raychem' Splice Removal on Containment Air Cooler Motor

Cables . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36

.7

Review of Calculation on the Electric Transient Analysis Profile . . . . . . 37

.8

Inadequate Grid Voltage Calculations . . . . . . . . . . . . . . . . . . . . . . . . . 38

(3)

Detailed Team Review of Licensee Corrective Actions Implemented to

Address Mechanical Issues Previously Identified by NRC or the Licensee

. . . 38

.1

High Pressure Injection Pump Operation Under Long Term

Minimum Flow . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39

.2

Increased Dose Consequences Due to Degraded Thermal

Performance Operation of Degraded Containment Air Coolers . . . . . . 42

.3

Containment Air Cooler Air Flow Calculation Concerns . . . . . . . . . . . . 43

.4

Accumulator Sizing Calculation Errors . . . . . . . . . . . . . . . . . . . . . . . . . 45

.5

Inadequate Blowdown Provisions for Containment Isolation Valve

Accumulators . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 47

.6

Non-conservative Calculation Used in Design Analysis to

Determine Required Service Water Makeup Flow to Component

Cooling Water . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 49

.7

Calculation Concerns for Service Water Pump Room Ventilation

System . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 50

.8

Inadequate Service Water System Flow Analysis . . . . . . . . . . . . . . . . . 52

.9

Inadequate Flooding Protection for the Service Water System

. . . . . . 53

.10

Inadequate Service Water System Flow Balance Testing

Procedure . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 55

.11

Service Water Discharge Path Swapover Setpoint . . . . . . . . . . . . . . . . 56

.12

Service Water Discharge Check Valve Test Acceptance Criteria . . . . . 59

.13

Lack of Design Basis Calculations to Support Service Water

Single Failure Assumptions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 61

.14

Auxiliary Feedwater System Calculation Issues With Main Steam

Safety Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 63

.15

Auxiliary Feedwater Strainer Mesh Size and Preconditioning of

Auxiliary Feedwater System During Testing . . . . . . . . . . . . . . . . . . . . . 64

.16

Inadequate Evaluation of System Health Condition Report on Auxiliary

Feedwater Design Bases Calculations . . . . . . . . . . . . . . . . . . . . . . . . . 67

.17

Containment Post-LOCA Trisodium Phosphate . . . . . . . . . . . . . . . . . . 68

.18

Borated Water Storage Tank Calculation Issues . . . . . . . . . . . . . . . . . 70

.19

Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover

Stud Overstressing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 72

.20

Reactor Coolant Pump Inner Gasket Leakage . . . . . . . . . . . . . . . . . . . 74

.21

Environmental Qualification of Equipment Not Supported by Analysis

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 75

.22

Inadequate Justification for Downgrade of Significant Condition

Adverse to Quality . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 77

.23

Inappropriate Application of 10 CFR 50.59 . . . . . . . . . . . . . . . . . . . . . . 78

Enclosure

iii

.24

Failure to Perform Comprehensive Moderate Energy Line Break

Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 81

(4)

Detailed Team Review of Licensee Corrective Actions Implemented to

Address Operational Issues Previously Identified by the Licensee . . . . . . . . . . 82

Repetitive Spacer Grid Strap Damage . . . . . . . . . . . . . . . . . . . . . . . . . 82

(5)

Review of Fire Protection Corrective Action Items . . . . . . . . . . . . . . . . . . . . . . 86

.1

Process Monitoring Function for Alternative Shutdown Capability . . . . 86

.2

Supporting Functions for Alternative Shutdown Capability . . . . . . . . . . 87

.3

Emergency Diesel Generator Floor Drains Design Deficiency . . . . . . . 88

(6)

Review of Licensee Event Reports

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 89

.1

(Discussed) LER 05000346/2002-008-00 and -01: Containment

Air Coolers Collective Significance of Degraded Conditions . . . . . . . . . 90

.2

(Closed) LER 05000346/2002-009-00: Degradation of the High

Pressure Injection Thermal Sleeves . . . . . . . . . . . . . . . . . . . . . . . . . . . 92

.3

(Closed) LER 05000346/2003-003-00 and -01: Potential

Inadequate High Pressure Injection Pump Minimum Recirculation

Flow Following a Small Break Loss of Coolant Accident

. . . . . . . . . . . 92

4OA4 Cross-Cutting Aspects of Findings

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 94

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95

(1)

Assessment of the Licensees Corrective Actions to Address Previously Identified

Findings Documented in NRC Reports . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95

.1

Follow up on Findings Documented in Report 05000346/2002012 . . . . . . . . . 95

.1

(Closed) URI 05000346/2002012-02: Potential Impact of

Corrosion on the Ground Function of Electrical Conduit in

Containment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 95

.2

(Closed) URI 05000346/2002012-03: Potential Failure to Follow

the Procedure for Raychem' Splice Removal on Electrical

Cables . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 96

.2

Follow-up on SSDI Findings Documented in Report 05000346/2002014 . . . . . 96

.1

(Discussed) NCV 05000346/2002014-01a: Lack of a Design

Basis Analysis for Containment Isolation Valve Backup Air

Supplies . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 96

.2

(Discussed) NCV 05000346/2002014-01b: Inadequate Blowdown

Provisions for Containment Air Cooler Backup Air Accumulators . . . . . 96

.3

(Closed) URI 05000346/2002014-01c: Failure to Perform

Comprehensive Moderate Energy Line Break Analysis . . . . . . . . . . . . 97

.4

(Closed) URI 05000346/2002014-01d: Lifting of Service Water

Relief Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 97

.5

(Closed) URI 05000346/2002014-01e: Inadequate Service Water

Pump Room Temperature Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . 97

Enclosure

iv

.6

(Closed) URI 05000346/2002014-01f: Inadequate Service Water

Pump Room Steam Line Break Analysis . . . . . . . . . . . . . . . . . . . . . . . 97

.7

(Closed) URI 05000346/2002014-01g: Inadequate Cable

Ampacity Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 97

.8

(Closed) URI 05000346/2002014-01h: Inadequate Flooding

Protection for Service Water Pump House . . . . . . . . . . . . . . . . . . . . . . 98

.9

(Discussed) NCV 05000346/2002014-01i: Non-conservative

Technical Specification Value for 90 Percent Undervoltage Relays . . . 98

.10

(Closed) URI 05000346/2002014-01j: Poor Quality Calculation for

90 Percent Undervoltage Relays . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 98

.11

(Discussed) NCV 05000346/2002014-01k: Non-conservative

Relay Setpoint Calculation for the 59 Percent Undervoltage

Relays . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 98

.12

(Closed) URI 05000346/2002014-01l: Inadequate Calculations for

Control Room Operator Dose (GDC-19) and Offsite Dose (10

CFR Part 100) Related to High Pressure Injection Pump Minimum

Flow Values . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 99

.13

(Closed) URI 05000346/2002014-01m: Other GDC-19 and 10

CFR Part 100 Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 99

.14

(Closed) URI 05000346/2002014-01n: High Pressure Injection

Pump Operation Under Long Term Minimum Flow . . . . . . . . . . . . . . . . 99

.15

(Closed) URI 05000346/2002014-01o: Some Small Break Loss of

Coolant Accident Sizes Not Analyzed . . . . . . . . . . . . . . . . . . . . . . . . . . 99

.16

(Closed) URI 05000346/2002014-01p: Inadequate Service Water

System Flow Analyses . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100

.17

(Closed) URI 05000346/2002014-01q: Inadequate Service Water

System Thermal Analyses . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100

.18

(Closed) URI 05000346/2002014-01r: Inadequate Ultimate Heat

Sink Inventory Analysis

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100

.19

(Closed) URI 05000346/2002014-01s: No Valid Service Water

Pump Net Positive Suction Head Analysis . . . . . . . . . . . . . . . . . . . . . 100

.20

(Closed) URI 05000346/2002014-01t: Service Water Source

Temperature Analysis for Auxiliary Feedwater . . . . . . . . . . . . . . . . . . 100

.21

(Closed) URI 05000346/2002014-01u: Inadequate Short Circuit

Calculations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100

.22

(Discussed) NCV 05000346/2002014-01v: No Analytical Basis for

Setpoint to Swap Service Water System Discharge Path . . . . . . . . . . 101

.23

(Discussed) NCV 05000346/2002014-02a: Service Water

Surveillance Test Did Not Use Worst Case Values

. . . . . . . . . . . . . . 101

.24

(Closed) URI 05000346/2002014-02b: Inadequate Service Water

Flow Balance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 101

.25

(Closed) URI 05000346/2002014-03a: Inappropriate Service

Water Pump Curve Allowable Degradation

. . . . . . . . . . . . . . . . . . . . 101

.26

(Closed) URI 05000346/2002014-03b: Repetitive Failures of

Service Water Relief Valves . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 102

.27

(Closed) URI 05000346/2002014-03c: Non-conservative

Difference in Ultimate Heat Sink Temperature Measurements . . . . . . 102

Enclosure

v

.28

(Discussed) NCV 05000346/2002014-03d: Inadequate Corrective

Actions Related to Service Water Pump Discharge Check Valve

Acceptance Criteria . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 103

.29

(Closed) URI 05000346/2002014-03e: Non-conservative

Containment Air Cooler Mechanical Stress Analysis . . . . . . . . . . . . . 103

.30

(Discussed) NCV 05000346/2002014-04: Failure to Perform

Technical Specification Surveillance for High Pressure Injection

Pump Following Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 103

.31

(Closed) URI 05000346/2002014-05: Question Regarding

Definition of a Passive Failure . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 104

.3

Follow-up on SSDI Findings Documented in Report 05000346/2002019 . . . . 104

(Closed) URI 05000346/2002019-031: Final Evaluation of

Apparent Cause Evaluation for LER 05000346/2002-006-00 . . . . . . . 104

.4

Follow up on Augmented Inspection Team Findings Documented in the

Cover Letter of Report 05000346/2003016 . . . . . . . . . . . . . . . . . . . . . . . . . . 104

.1

(Discussed) AV 05000346/2003016-01: Technical Specification

Reactor Coolant System Pressure Boundary Leakage . . . . . . . . . . . . 104

.2

(Discussed) AV 05000346/2003016-02: Reactor Vessel Head

Boric Acid Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 105

.3

(Discussed) AV 05000346/2003016-03: Containment Air Cooler

Boric Acid Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 107

.4

(Discussed) AV 05000346/2003016-04: Radiation Filter Element

Deposits . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 107

.5

(Discussed) AV 05000346/2003016-05: Service Structure

Modification Delay . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 107

.6

(Discussed) AV 05000346/2003016-06: Reactor Coolant System

Unidentified Leakage Trend . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 109

.7

(Discussed) AV 05000346/2003016-07: Inadequate Boric Acid

Corrosion Control Program Procedure . . . . . . . . . . . . . . . . . . . . . . . . 110

.8

(Discussed) AV 05000346/2003016-08: Failure to Follow Boric

Acid Corrosion Control Program Procedure . . . . . . . . . . . . . . . . . . . . 110

.9

(Discussed) AV 05000346/2003016-09: Failure to Follow

Corrective Action Program Procedure . . . . . . . . . . . . . . . . . . . . . . . . 112

(2)

Closure of Restart Checklist Items

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 112

.1

Restart Checklist Item 2.c: Structures, Systems, and

Components Inside Containment . . . . . . . . . . . . . . . . . . . . . . . . . . . . 112

.2

Restart Checklist Item 3.a: Corrective Action Program . . . . . . . . . . . 113

.3

Restart Checklist Item 5.b: Systems Readiness for Restart

. . . . . . . 113

4OA6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 114

Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 114

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A1

Enclosure

vi

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

. . . . . . . . . . . . . . . . . . . . . A2

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A7

LIST OF ACRONYMS USED

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A39

Enclosure

SUMMARY OF FINDINGS

IR 05000346/2003010(DRS); 03/17/2003 - 01/07/2004; Davis-Besse Nuclear Power Station;

Corrective Action Program Implementation Effectiveness

The inspection consisted of five weeks of on-site activities over a six month period. The

specific on-site weeks were the weeks of: March 17, March 31, May 18, August 11, and

August 25, 2003. This report documents a special corrective action program implementation

team inspection. The inspection was conducted to assess the adequacy of the licensees

implementation of the facilitys corrective action program. The inspection was conducted by

regional engineering inspectors and supplemented by consultants. Two Green findings

associated with two cited violations, one Severity Level IV Non-Cited Violation (NCV), and

twenty-six (26) Green findings associated with 26 NCVs were identified.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

NRC Inspection Manual Chapter 0609, "Significance Determination Process." Findings for

which the significance determination process does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor

Oversight Process," Revision 3, July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix R,

Section III.L.2.d, having very low safety significance. Specifically, the licensee failed to

provide the process monitoring function, capable of providing direct readings of the

process variables necessary to perform and control the alternative shutdown, for a

control room or cable spreading room fire. Following discovery, the licensee entered the

issue into the corrective action program and performed a modification to resolve the

issue. The primary cause of this violation was related to the cross-cutting area of

problem identification and resolution because the licensee had previously identified this

issue as an enhancement and did not recognize that it was a violation of regulatory

requirements.

This issue was more than minor because it affected the initiating events cornerstone

and, by not providing the direct indications necessary for the operators to determine the

status of the idle SG, the probability of experiencing unacceptable stresses on the SG

tubes during the limiting Appendix R scenario was increased. The team determined this

finding to be of very low significance, based upon the low probability of a serious control

room fire combined with the low probability that such a fire would affect this specific

instrumentation detrimentally. Additionally, even in the event that such a fire had

affected this instrumentation, it was likely that the operators still would have been able to

prevent these tube stresses through use of manual actions, although this was not a

credited action in the Fire Protection procedures for this scenario. (Section 4OA3(5)b.1)

Enclosure

2

Cornerstone: Mitigating Systems

Green. The team identified a Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control. Specifically, the licensee failed to provide a basis for the

setpoint to swap the service water system discharge path. This issue was previously

identified as a Non-Cited Violation in Inspection Report 05000346/2002014 and the

corrective actions taken by the licensee failed to correct the originally identified

condition. The primary cause of this violation was related to the cross-cutting areas of

problem identification and resolution and human performance, because the licensee did

not recognize that the corrective actions taken needed to restore compliance with the

identified violation of NRC requirements.

The issue was determined to be more than minor because the licensee had not

corrected a previous violation and was relying on non-safety-related equipment to

perform a safety function under design bases conditions. Because the issue was

previously determined to be of very low safety significance, NRC management

concluded that the violation could be categorized as having very low safety significance.

(Section 4OA3(3)b.11)

Green. The team identified a Cited Violation of Technical Specifications Section 4.05a

and 10 CFR 50.55a. Specifically, the licensee failed to ensure that the service water

discharge check valve was tested in accordance with the American Society of

Mechanical Engineers Code. The primary cause of this violation was related to the

cross-cutting areas of problem identification and resolution and human performance,

because the licensee did not recognize that the corrective actions taken needed to

ensure compliance with NRC requirements.

The issue was determined to be more than minor because the inadequate test

acceptance criteria allowed the licensee to accept a check valve as performing its

intended function at less than full system flow. The issue was of very low safety

significance using the Phase 1 of the significance determination process based on the

licensees determination that the system was operable but degraded.

(Section 4OA3(3)b.12)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to translate instrument uncertainties into the undervoltage time delay

setting specification for the 4160 Vac buses C1 and D1. Following discovery, the

licensee confirmed the settings were acceptable and re-evaluated the potential

temperature effects to the time delay relays.

This issue was more than minor because the licensee had to perform calculations to

show that the relays were within their allowable values, and because the licensee

determined that the increased temperature could cause the time delay to operate

outside of Technical Specifications limits. The issue was of very low safety significance

using the Phase 1 of the significance determination process since the licensee

considered the instruments to be operable. (Section 4OA3(2)b.1)

Enclosure

3

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to provide motor thermal overload protection for the Class 1E 480

alternating current voltage (Vac) distribution system. Following discovery, the licensee

physically modified approximately 53 thermal overload circuits to resolve the

discrepancy. The primary cause of this violation was related to the cross-cutting area of

human performance because the licensee did not realize the lack of thermal overload

protection was an unanalyzed condition and that the station was not in compliance with

the updated safety analysis report until identified by the team.

This issue was more than minor because the licensee failed to ensure that bypassing

the thermal overload protection would result in completion of safety functions and

subsequently had to install thermal overload protection in order to meet the design

requirement. The issue was determined to be of very low safety significance using

Phase 1 of the significance determination process because there was reasonable

assurance that the condition did not result in a loss of system function. (Section

4OA3(2)b.2)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XI, Test Control, having very low safety significance. Specifically, the

licensee failed to adequately test direct current contactors related to two safety related

motor operated steam valves associated with the auxiliary feedwater system. Following

discovery, the licensee entered the issue into the corrective action program and was

re-evaluating the basis for acceptability of these valves. The primary cause of this

violation was related to the cross-cutting area of problem identification and resolution

because, although the issue was identified in 2002, the licensee did not see the need to

take corrective action until prompted by the team in 2003.

This issue was more than minor because the licensee had relied upon an inadequate

test to show that the contactors were qualified to perform under required conditions and

because the contactors were installed in the plant during previous operating cycles. The

issue was of very low safety significance using the Phase 1 of the significance

determination process because the licensee determined that the valves were operable.

(Section 4OA3(2)b.3)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, having very low safety significance. Specifically, the

licensee failed to identify and correct inadequate short circuit protection for direct current

(DC) circuits. Following discovery, the licensee issued a condition report to document

the deficient circuit protection for valves with extremely long circuit lengths. The primary

cause of this violation was related to the cross-cutting area of problem identification and

resolution because the licensee had missed several opportunities to identify it as part of

corrective actions for previously identified DC circuit deficiencies.

This issue was more than minor because the licensee had to perform calculations to

show that the fuses would adequately protect the equipment and because modifications

to those fuses were required. The issue was of very low safety significance using

Phase 1 of the significance determination process because the licensee concluded the

equipment was operable. (Section 4OA3(2)b.4)

Enclosure

4

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to confirm operability of direct current (DC) contactors by ensuring that

minimum voltage was available at the safety related device terminals. The licensee

missed several opportunities to correct this design deficiency. Following discovery, the

licensee issued a condition report to evaluate the adequacy of available voltage. The

primary cause of this violation was related to the cross-cutting area of problem

identification and resolution because, although the issue was identified in 2002, the

licensee did not see the need to take corrective action until prompted by the team in

2003.

This issue was more than minor because the licensee had to perform calculations to

determine if the devices had sufficient voltage to perform their safety function. The

issue was of very low safety significance using Phase 1 of the significance

determination process because the licensee determined that all components were

operable. (Section 4OA3(2)b.5)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to verify that the high pressure injection pumps could operate under

design basis minimum flow requirements since initial plant startup. The primary cause

of this violation was related to the cross-cutting area of problem identification and

resolution because the licensee missed several opportunities to identify and correct the

deficiency.

This issue was more than minor because the licensee had to perform a test to

demonstrate that design basis requirements could be met and because the test results

determined that the design basis requirements needed to be changed to ensure that the

HPI pumps could perform their accident required function. The issue was of very low

safety significance because surveillance test results indicated the lowest flow rate for

either pump was slightly outside the licensee's new operability band, and therefore, it

was deemed likely that the pumps would have performed had they been called upon.

The issue screened out of Phase 1 of the significance determination process.

(Section 4OA3(3)b.1)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to consider worst case minimum pressure differential between service

water and component cooling water systems when determining required service water

makeup flow to the component cooling water system heat exchangers. Following

discovery, the licensee entered the issue into the corrective action program and

performed the necessary calculations. The primary cause of this violation was related to

the cross-cutting area of human performance because the licensee used test data

collected during normal operation rather than taking the worst case design conditions

and because there was a lack of rigor in the calculation review process.

This issue was more than minor because the licensee needed to perform a new

calculation to demonstrate that the service water flow to the component cooling water

Enclosure

5

system was adequate to perform its design function under accident conditions. The

issue was of very low safety significance because the licensee determined the system

was operable. Therefore, the issue screened out of Phase 1 of the significance

determination process. (Section 4OA3(3)b.6)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to verify the adequacy of the design of the service water (SW) pump

room ventilation system. Following discovery that the design basis calculations were

non-conservative, the licensee entered the issue into the corrective action program,

re-performed the calculations, and made appropriate modifications to correct the issues.

The primary cause of this violation was related to the cross-cutting area of corrective

action because the licensee failed to correct all of the originally identified issues until

identified by team.

This issue was more than minor because inadequacies in the calculations resulted in a

modification which was required to ensure winter operation was within the allowable

temperature range, and because the revised calculation did not include all the summer

heat loads which could potentially impair the SW pump room ventilation system to

perform its safety function. The issue was of very low safety significance because the

licensee determined that past non-procedurally-required compensatory actions had

prevented the equipment from actually being inoperable. Therefore, the issue screened

out of Phase 1 of the significance determination process. (Section 4OA3(3)b.7)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to ensure that the service water system could perform its design function

under all required conditions. Following discovery, the licensee documented the issue in

the corrective action program and performed the necessary calculations.

This issue was more than minor because the licensee did not initially have a calculation

which showed that the service water (SW) system could fulfill its design function under

design basis conditions and because, when the calculation was prepared, it identified

circumstances where the system would not be able to perform its safety function and

those circumstances were not evaluated to ensure that the safety function could be met.

The issue was of very low safety significance because the licensee concluded that the

SW system had never been unable to perform its safety function. Therefore, the issue

screened out of Phase 1 of the significance determination process.

(Section 4OA3(3)b.8)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to have provisions in place to protect the service water pump room from

flooding. Following discovery, the licensee placed the issue in the corrective action

program, evaluated the issue and established procedures to address the issue.

This issue was more than minor because the licensee had to make procedural changes

in order to ensure that safety-related equipment was capable of performing its safety

functions. The issue was of very low safety significance because the deficiency only

Enclosure

6

dealt with a lack of procedural guidance. Therefore, the issue screened out of Phase 1

of the significance determination process. (Section 4OA3(3)b.9)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XI, Test Control, having very low safety significance. Specifically, the

licensee failed to account for a number of conditions in the service water system flow

balance testing procedures. Following discovery, the licensee placed the issue in the

corrective action program, evaluated the issue and established procedures to address

the issue.

This issue was more than minor because procedural changes were necessary in order

to ensure that the safety-related service water (SW) system branch flow rates were

adequate for the system to perform its safety functions. The issue was of very low

safety significance because the licensee concluded that the system was previously

capable of meeting its design requirements. Therefore, the issue screened out of

Phase 1 of the significance determination process. (Section 4OA3(3)b.10)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to provide an analysis which addressed the service water valve single

failure assumptions described in the updated safety analysis report. Following

discovery, the licensee entered the issue in the corrective action program. The primary

cause of this violation was related to the cross-cutting area of problem identification and

resolution because the licensee had not recognized the impact of the issue on the

design basis and had not corrected it after it was identified in 2002.

This issue was more than minor because the current calculations were non-conservative

and the licensee was not able to show that the service water system could perform its

safety function under design basis conditions. The issue was of very low safety

significance because the team determined that it was unlikely that the service water

system would not function during a design basis accident, as there would need to be a

maximum service water temperature or minimum ultimate heat sink level and a specific

valve single failure. This issue was a design deficiency that would not likely result in the

loss of function; therefore, the issue screened out of Phase 1 of the significance

determination process. (Section 4OA3(3)b.13)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to ensure that design analyses showed that the auxiliary feedwater

(AFW) system could perform its safety function under design basis conditions.

Following discovery, the licensee entered the issue into the corrective action program.

The primary cause of this violation was related to the cross-cutting area of human

performance, as the licensee used the results of a vendor calculation without verifying

that it was adequate.

This issue was more than minor because the calculations were non-conservative and

the calculation of record did not demonstrate that the AFW system could perform its

safety function under design basis conditions. Based on further analysis, the licensee

concluded the AFW system was operable. Therefore, the issue screened out of

Phase 1 of the significance determination process and was of very low safety

significance. (Section 4OA3(3)b.14)

Enclosure

7

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XI, Test Control, having very low safety significance. Specifically, the

licensee failed to recognize that flushing the system and blowing down the strainers

upstream of the turbine driven pump bearing cooling water strainers prior to routine

surveillances constituted preconditioning of the auxiliary feedwater system. Following

discovery, the licensee entered the issue into the corrective action program. The

primary cause of this violation was related to the cross-cutting area of problem

identification and resolution because the licensee had failed to recognize the

consequences of the preconditioning when evaluating an earlier issue.

This issue was more than minor because there was not sufficient information to show

that test requirements would have been met had the strainers not been blown down.

The issue was of very low safety significance because the licensee considered the

system operable. Therefore, the issue screened out of Phase 1 of the significance

determination process. (Section 4OA3(3)b.15)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, having very low safety significance. Specifically, the

licensee failed to ensure that emergency core cooling system pump motors were

environmentally qualified for the stated mission time, as stated in a license amendment

request submitted to the NRC. Following discovery, the licensee entered the issue into

the corrective action program. The primary cause of this violation was related to the

cross-cutting area of human performance as the licensee did not ensure that personnel

developing license documents had the necessary information.

This issue was more than minor because, if left uncorrected, this weakness could result

in a repeat failure of the corrective action program to adequately identify, evaluate and

correct problems. The issue was of very low safety significance because the licensee

considered that the motors could be environmentally qualified. Therefore, the issue

screened out of Phase 1 of the significance determination process.

(Section 4OA3(3)b.21)

Severity Level IV. The team identified a Non-Cited Violation of 10 CFR 50.59,

Changes, Tests and Experiments. Specifically, the licensee failed to preform an

adequate evaluation of a defacto modification to the plant where the underlying change

may have required NRC approval prior to implementation. The design change involved

degraded or missing physical barriers that could result in one or more of the diesel

generators failing to fulfill their design function during a tornado. Following discovery,

the licensee entered the issue into the corrective action program and re-performed the

analysis. The licensee also repaired those barriers which were physically degraded.

The primary cause of this violation was related to the cross-cutting area of human

performance as the licensee appeared to selectively choose information from the

guidance document in order to achieve the desired outcome.

Because this issue affected the NRCs ability to perform its regulatory function, this

finding was evaluated with the traditional enforcement process. The finding was

determined to be of very low safety significance based on a significance determination

Enclosure

8

process analysis of a loss of offsite power concurrent with loss of one emergency diesel

generator. (Section 4OA3(3)b.23)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to include environmental effects of a decay heat removal pump seal

failure in the moderate energy line break analysis. Following discovery, the licensee

entered the issue into the corrective action program and re-performed the analysis.

This issue was more than minor because the licensee had to perform calculations to

show that the environmental effects were acceptable. The issue was of very low safety

significance because, upon completing the analysis, the licensee determined that the

moderate energy line break heat loads were acceptable and that the system could

perform its design function. Therefore, the issue screened out of Phase 1 of the

significance determination process. (Section 4OA3(3)b.24)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Section III.L.2.e,

having very low safety significance. Specifically, the licensee failed to provide the

process cooling and lubrication necessary to permit the operation of the equipment used

for safe shutdown functions. Following discovery, the licensee entered the issue into

the corrective action program and performed a modification to resolve the issue. The

primary cause of this violation was related to the cross-cutting area of problem

identification and resolution because the licensee had previously identified this issue as

an enhancement and did not recognize that it was a violation of regulatory requirements.

This issue was more than minor because, if left uncorrected, the finding would become

a more significant safety concern. By not providing containment air cooling as per the

governing alternative shutdown procedure, the probability of the failure of equipment

relied upon for safe shutdown was increased. This issue was screened to be of very low

safety significance because there was not a total loss of safety function for an assumed

control room fire with evacuation. (Section 4OA3(5)b.2)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50.48(a)(1), having

very low safety significance. Specifically, the licensee failed to evaluate the adequacy of

emergency diesel generator common floor drains following sprinkler system actuation in

the fire affected emergency diesel generator room. Following discovery, the licensee

entered the issue into the corrective action program and revised the fire response

procedures to address the issue.

This issue was more than minor because it affected the mitigating systems cornerstone

and the potential existed that a fire in one emergency diesel generator room would

potentially impact the redundant emergency diesel generator following sprinkler actuation

in the fire affected emergency diesel generator room. The finding was of very low safety

significance since this issue was a design deficiency that was confirmed not to result in

the loss if function per Generic Letter 91-18, Revision 1. Therefore, the issue screened

out of Phase 1 of the significance determination process. (Section 4OA3(5)b.3)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

Enclosure

9

licensee failed to provide for the original plant design to incorporate a safety-related

recirculation path for the high pressure injection (HPI) pumps in the high pressure

recirculation (HPR) mode of operation. Following discovery, the licensee installed an

additional minimum flow recirculation line for each HPI pump.

This issue was more than minor because the original plant design did not incorporate a

safety-related recirculation path for the HPI pumps in the HPR mode of operation and

this finding affected the mitigating systems cornerstone. The issue was of very low

safety significance because the HPR safety-function would not actually have been lost

because of existing procedure actions for feed and bleed operations in situations where

the steam generators could not be used to remove decay heat. Therefore, the finding

screened out as having very low safety significance. Section (4OA3(6)b.3)

Cornerstone: Barrier Integrity

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to correctly identify and translate the design basis requirements into the

containment air coolers airflow analyses and motor horsepower sizing calculations. The

primary cause of this violation was related to the cross-cutting area of problem

identification and resolution as the licensee had previously identified issues with the

motors, but had not reviewed the design calculation of record. Following discovery, the

licensee entered the issue into the corrective action program and performed a new

analysis for the motor.

This issue was more than minor because the licensee had to revise the associated

calculation to evaluate the existing motor to ensure the containment air coolers (CAC)

would be able to perform their design function. The issue was evaluated in a Phase 1

analysis in the significance determination process. Because the issue involved both the

mitigating system and barrier integrity cornerstones, a Phase 2 analysis was also

performed. A final evaluation was obtained that the issue was of very low safety

significance. (Section 4OA3(3)b.3)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to evaluate a potential overstressing condition on the reactor coolant

pump casing-to-cover studs. Following discovery, the licensee entered the issue into

the corrective action program. The primary cause of this violation was related to the

cross-cutting area of problem identification and resolution as the licensee closed a

condition report without recognizing that the apparent condition adverse to quality had

not been addressed.

This issue was more than minor because the NRC had to perform calculations to

determine if the reactor coolant pump studs were within ASME Code allowables. The

issue was of very low safety significance based on the NRC determination that the studs

were always functional. Therefore, the issue screened out of the Phase 1 significance

determination process as having very low safety significance. (Section 4OA3(3)b.19)

Enclosure

10

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion XVI, Corrective Action, having very low safety significance. Specifically, the

licensee failed to take adequate corrective actions to previous events to prevent

damage to a new fuel assembly spacer grid strap during the final reload of the core in

February 2003. Following discovery, the licensee entered the issue into the corrective

action program. The primary cause of this violation was related to the cross-cutting

areas of corrective action and human performance, because, despite earlier events, the

licensee failed to adequately address the human performance issues that contributed to

this and other fuel spacer grid events.

This issue was more than minor because the licensee failed to prevent recurrence of a

significant condition adverse to quality resulting in damage occurring to previously

undamaged fuel assembly grid straps. The issue only involved the fuel barrier and it

screened out of the Phase 1 significance determination process as having very low

safety significance. (Section 4OA3(4)b)

Non-Significance Determination Process Issues

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to assess an increase in the offsite dose to the public following a

postulated design basis accident due to increased containment pressure. Following

discovery, the licensee entered the issue into the corrective action program and

performed the necessary analysis. The primary cause of this violation was related to

the cross-cutting area of problem identification and resolution, because, although the

issue had been previously identified, the licensee had failed to identify that a revised

dose assessment was needed until prompted by the NRC.

This issue was more than minor because the licensee had to perform calculations to

show that the increased time at higher containment pressures did not result in doses

being above regulatory guide allowables. The mitigating system cornerstone was not

affected since the finding pertained to offsite dose calculations rather than containment

air coolers performance. Based on this review, the team determined that the issue was

not covered by any of the revised oversight cornerstones and was, therefore, not

suitable for SDP analysis. This determination was due to the issue regarded

containment pressure and related to offsite dose consequences. Regional management

determined that this regulatory issue was of very low safety significance because

projected offsite doses remained less than Regulatory Guide 1.4 allowances.

(Section 4OA3(3)b.2)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to implement effective design control measures to check and verify the

adequacy of the design basis calculation performed for sizing the new accumulators

used to hold the service water containment isolation valves closed on a loss of

instrument air. Following discovery, the licensee entered the issue into the corrective

action program, revised calculations, and changed the accumulator medium from

compressed air to nitrogen.

Enclosure

11

This issue was more than minor because the licensee had to change the modification

design from having accumulators containing pressurized air to accumulators containing

pressurized nitrogen. This finding was evaluated in Phase 1 of the significance

determination process. The mitigating system cornerstone was not affected since the

finding pertained to the sizing of accumulators associated with containment isolation

valves. Therefore, the issue was not covered by any of the revised oversight

cornerstones and was, therefore, not suitable for SDP analysis. This determination was

based on the issue affecting containment isolation valves which provide a barrier to

breach of containment and potential offsite dose consequences. Regional management

determined that this regulatory issue was of very low safety significance.

(Section 4OA3(3)b.4)

Green. The team identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, having very low safety significance. Specifically, the

licensee failed to translate the postulated radiological consequences of leakage from

engineered safety feature components outside containment into calculations of record

for post-accident control room dose and offsite boundary dose. Following discovery, the

licensee entered the issue into the corrective action program and provided a bounding

evaluation which demonstrated that the increase in dose was within acceptable limits.

This issue was more than minor because the licensee had to perform calculations to

show that the increased doses remained within the post accident dose level

requirements. The issue could not be assessed through the significance determination

process, because none of the cornerstone objectives addressed design issues dealing

with postulated doses following a design basis accident. After determination that the

increase in dose did not involve an issue requiring a license amendment, Regional

Management concluded the regulatory issue was of very low safety significance.

(Section 4OA3(3)b.18)

B.

Licensee-Identified Violations

No findings of significance were identified.

Enclosure

12

REPORT DETAILS

4.

OTHER ACTIVITIES (OA)

4OA2 Identification and Resolution of Problems (71152B)

Background

On March 6, 2002, Davis-Besse personnel notified the NRC of degradation (corrosion)

of the reactor vessel head material adjacent to a control rod drive mechanism (CRDM)

nozzle. This condition was caused by coolant leakage and boric acid corrosion of the

head material induced by an undetected crack in the adjacent CRDM nozzle. The

degraded area covered in excess of 20 square inches where the low-alloy carbon

structural steel was corroded away, leaving the thin stainless steel cladding layer. This

condition represented a loss of the reactor vessels pressure retaining design function,

since the cladding was not considered as pressure boundary material in the structural

design of the reactor pressure vessel. While the cladding did provide a pressure

retaining capability during reactor operations, the identified degradation represented an

unacceptable reduction in the margin of safety of one of the three principal fission

product barriers at Davis-Besse. This issue was documented in inspection report (IR)

05000346/2002003. The event was captured in the licensee's corrective action program

(CAP) as condition report (CR) 02-00891, "Failure to Identify Significant Degradation of

the Reactor Pressure Vessel Head." The root cause analysis report for the CR

documented that one of the root causes of the event was "less than adequate

implementation of the corrective action program."

As part of the licensees return to service plan and as corrective action for the

circumstances that led to the vessel head degradation, the licensee implemented the

Davis-Besse system health assurance (SHA) plan. This plan described activities to

review plant systems prior to restart to ensure that plant systems were in a condition

that would support safe and reliable operation.

In an effort to identify adverse trends and problem areas, the licensee performed a

collective review of approximately 600 relatively significant CRs and developed

approaches to correct the discrepancies, evaluate the extent of condition, address any

trends, and resolve the issues. The licensee used a three-phase corrective action

process to identify and resolve deficiencies:

Path A - Resolution of each condition identified and determination of the extent

of condition. This approach used the stations CAP to determine cause, extent

of condition, and implement specific corrective actions for discrepancies

Path B - Evaluation to provide additional assurance of significant safety function

capabilities. The collective review identified numerous deficiencies in the areas

of calculations and testing which validated or verified the capability of safety

systems to perform their functions.

Enclosure

13

Path C - Resolution of design-related programmatic issues. The collective

review identified numerous discrepancies in five design-related programmatic

areas (station flooding, high energy line break, environmental qualification,

seismic qualification, and 10 CFR Part 50, Appendix R - Safe Shutdown) within

each of the five systems selected for a detailed latent issues review. The

licensee conducted a specific detailed examination of CRs to identify,

characterize, determine the extent of condition, and correct the problems in each

of those programmatic areas.

The licensees review efforts identified numerous discrepancies involving an inadequate

CAP, inadequate configuration control, degraded hardware conditions, inconsistent and

potentially non-conservative assumptions in design basis and licensing basis

documents, deficient or unavailable calculations, and non-conservative operating and

test procedures which did not reflect design and licensing basis documents. The

identified discrepancies were documented in new CRs and these CRs were assessed

for operability impact and significance in accordance with the stations CAP.

As part of the NRCs inspection of the SHA plan, a safety system design and

performance capability inspection (SSDI) was conducted on three systems: the service

water (SW), high pressure injection (HPI), and 4160 volt alternating current (AC)

electrical distribution systems. This inspection identified numerous deficiencies, which

mirrored the licensee's findings in a number of areas. This inspection, and the resultant

findings, were documented in IR 05000346/2002014.

(1)

Corrective Action Program Implementation

a.

Inspection Scope

To assess the licensees corrective actions to adequately address the numerous plant

deficiencies identified in 2002 during the licensees and NRC reviews, the NRC

conducted an in-depth corrective action team inspection (CATI) of the CAP

implementation. This inspection was intended to assess the effectiveness of the

licensees actions to identify the deficiencies, evaluate the cause(s) and correct the

problems in order to prevent recurrence.

In order to make the above assessment, the team reviewed selected CRs which

evaluated the licensees actions to address deficiencies documented in licensee event

reports (LERs), NRC Non-Cited Violations (NCVs), and NRC unresolved items (URIs)

from previous inspections. The selected CRs also involved issues identified by the

licensee as part of their system health readiness or latent issue reviews. The team's

focus was on CRs which the licensee had identified as requiring resolution prior to the

restart of the plant, with a further emphasis on those CRs which the licensee had

determined to be "significant conditions adverse to quality (SCAQ)."

The team specifically assessed the licensee's CAP in four separate areas:

Identifying problems; including recognizing performance issues within the CAP

itself;

Enclosure

14

Categorizing and prioritizing problems, with a specific emphasis on the licensee's

use of a process termed as "rollovers";

Evaluating those problems; including assessing root and apparent causes,

extent of conditions, operability and reportability;

Correcting problems, including not only the originally identified problem but any

issues identified as part of the evaluation, assessment of effectiveness of the

corrective actions and actions taken to prevent recurrence.

In addition, the team assessed two areas where a number of problems were identified.

These were:

Engineering Resolution of Design Deficiencies and

Procedure Quality and Adherence

b.

Observations and Findings

The corrective action program was described in procedure NOP-LP-2001, "Condition

Report Process." This procedure was significantly revised in March 2003, and again in

May 2003. The CAP consisted of a process to identify and resolve potential adverse or

undesirable conditions. It included issues, concerns, observations, equipment

deficiencies, human performance problems, equipment failures and programmatic

deficiencies.

The team began its inspection in March 2003. However, due to the licensee not being

ready for the inspection at that time, the inspection was delayed until May 2003, and the

most effective inspection actually occurred in August 2003, when the licensee had

completed sufficient packages for the team to review.

As described below, at the conclusion of the inspection, the team determined that,

overall, the licensee's program for identifying, prioritizing, evaluating, and correcting

performance deficiencies was acceptable. However, the team also observed that the

licensees actions to identify non-conforming issues and prevent recurrence were often

minimally effective. The team also identified evaluations which were narrowly focused

and not probing in nature. Consequently, the resulting corrective actions were also

narrowly focused. In areas where the licensee had established corrective actions, the

effectiveness of these actions could not be readily determined at the end of the

inspection due to the short time frame since implementation.

During the inspection, the team reviewed approximately 150 CRs. Of these, the team

determined that approximately 120 had weaknesses or deficiencies, of some type. As a

result of the teams findings, the licensee initiated approximately 120 additional CRs to

document and address the teams findings. Overall, the team determined that

approximately 80 percent of the CRs actually reviewed by the team had weaknesses or

deficiencies to some degree. The weaknesses and deficiencies identified by the team

resulted in the identification of findings documented in this inspection report.

Subsequent to the onsite inspection, on November 12 and December 10, 2003, the

licensee presented to the NRC, the planned actions to address the issues and concerns

identified by the CATI. As part of these meetings, the licensee made a number of

Enclosure

15

commitments to further improve the CAP as part of its Operational Improvement Plan

for Cycle 14, Revision 3. The team recognized that the improvement plan described

actions that should address the teams areas of concerns. Additionally, the licensee

implemented some improvements in the CAP. Examples included the revised CAP

procedure and the newly established CR analyst positions.

.1

Adequacy of Licensee's Efforts to Identify and Document Problems

The team determined that the licensee, overall, was adequately identifying and

documenting problems. However, a number of examples were identified where the

licensee had failed to identify or to document problems, particularly in the area of

design-related deficiencies. The team attributed these issues to a lack of attention to

detail, weak knowledge of system design basis, and a failure to follow CAP procedures.

Specific examples are listed below, and the more significant ones are discussed in

Sections 4OA3(2) and 4OA3(3) of this report.

Failure to identify the lack of thermal overload protection for safety related

motors (See Section 4OA3(2)b.2 for additional details);

Failure to identify oversized fuses in safety related motor operated circuits (See

Section 4OA3(2)b.4 for additional details);

Failure to identify the main steam safety valve (MSSV) setpoint drift and

accumulation, and the potential affect on auxiliary feedwater (AFW) pump flow

(See Section 4OA3(3)b.14 for additional details);

Failure to identify potential design problems with the containment air coolers

(CACs) (See Sections 4OA3(3)b.2 and 4OA3(3)b.3 for additional details);

Failure to write a CR for SW calculational deficiencies. (See CR 03-03977);

Failure to generate a CR to address a problem identified during the SSDI and

which was documented in that IR as NCV 02-014-01b (See Section 4OA3(3)b.5

for additional details);

Failure to identify lack of breaker coordination (CR 03-03572); and

Failure to identify configuration control discrepancies (CR 03-02699).

.2

Adequacy of Licensee's Efforts to Categorize and Prioritize Problems

The team determined that the licensee, overall, was adequately categorizing items in

regard to their safety significance and impact upon plant operation. The licensee also

generally appeared to be assigning an appropriate priority both to performing evaluations

and completing corrective actions prior to restart of the plant.

However, early in the inspections the team did identify a concern with a process the

licensee was using as part of their categorization process. This process, referred to as

"rollovers, allowed the licensee to disposition CRs by transferring either a portion or the

Enclosure

16

entire issue to one or more additional other open CRs. The licensee did place a

condition that the "rolled-into" CRs had to be of equal or greater category and had to

address the same issues. However, the issues described in the "rolled-out-of" CRs could

be broken into several different "rolled-into" CRs and "rolling" could occur on multiple

occasions (i.e., CR 1 was rolled into CR 2 which was rolled into CR 3, which then rolled

out part of CR 1s issues to CR 4...). This was especially true in regard to specified

corrective actions. As an example, the team identified that more than 25 corrective

actions were rolled over into CRs 02-00891, "Failure to Identify Significant Degradation of

the Reactor Pressure Vessel Head," and CR 02-04884, "Ineffective Corrective Action

Problem Resolution." Some problems were identified, and the extent of the rollover

process early in the inspection made it extremely difficult for the team to accurately

assess whether the overall process was adequately controlled and that corrective actions

were effectively implemented.

The team also noted that the CAP defined that a CR should only be listed as "closed"

when the evaluation was completed and all corrective actions were implemented.

However, the licensee frequently classified a "rolled out of" CR as "Closed", because the

evaluation and/or the corrective actions were transferred to another CR. This gave a

somewhat artificial characterization as to the status of resolution of identified issues.

The team was concerned that the complexity of the rollover process, the inability to

easily track resolution of identified concerns, and the lack of adequate guidance could

have resulted in inappropriate resolution of problems. Other examples of rollover

problems included: improper implementation of corrective actions, lack of cross

references and flawed cause analysis.

Specific examples of rollover problems identified by the team are listed below, and the

more significant ones are discussed in Sections 4OA3(2) and 4OA3(3) of this report.

The resolution to the trisodium phosphate (TSP) post-accident concerns were

difficult to evaluate due to the number of rollovers (See Section 4OA3(3)b.17 for

details);

Three CRs on fuel spacer grid damage were rolled into a SCAQ CR, but were

not addressed in the root cause analysis (See Section 4OA3(4)b for details);

Corrective action 13 in CR 02-05385 was not related to the identified issue.

Licensee determined that, due to rollovers, the corrective action ended up in the

wrong CR (CR 02-05385);

There were informal rollovers in CRs 02-07657, 02-05904, 02-05881, and

02-06779 (See Sections 4OA3(3)b.12, 4OA3(3)b.16, and 4OA3(3)b.19 for

further discussions regarding rollovers); and

In addition there was an inadequate rollover of overload protection concerns in

CR 03-02616 to CR 03-03572 (Section 4OA3(2)b.2).

The team identified that the licensee had issued seventeen CRs within a six month

period related specifically to licensee-identified concerns with the rollover process. As a

result of the team's review of rollover CRs, the licensee identified a specific issue, as

Enclosure

17

documented in CR 03-01955, "CR Rollover Discrepancies," regarding rollover of

concerns as part of the containment health review.

Based on both the team's and the licensees own internal findings in regard to the

rollover process, the licensee revised the CAP procedure to place limits on the number

of times an issue could be rolled and to strengthen the rollover process.

.3

Adequacy of Licensee's Efforts to Evaluate Identified Conditions

During the inspection, the team found examples where the licensee was not fully

effective in evaluating problems, particularly in regard to determining the apparent cause

of issues. The team determined that this failure to adequately evaluate issues could be

attributed to a narrow evaluation focus, weak knowledge of the design basis, and lack

of attention to detail.

At the start of the inspection, the licensee divided CR evaluations into three categories:

SCAQ CRs, which required a root cause evaluation; "CA" CRs which required an

apparent cause evaluation; and "CF" CRs which required the deficiency to be fixed and

did not require a cause evaluation.

While generally adequate, the team determined that some root cause evaluations did

not always use a formal method to arrive at a root cause. In at least one case, the root

cause did not arrive at a cause for the discrepant condition. In another, information

used to arrive at the conclusion was not discussed in the evaluation. In contrast, the

team identified that the root cause evaluation for SCAQ CR 02-00891, performed to

determine root and contributing causes of the head event, was well done.

In regard to the apparent causes, the team identified that the majority of the stated

apparent causes were one-line sentences and appeared to address the symptoms of

the deficiency and did not address why the condition happened.

The team noted that the CAP listed timeliness expectations as to when the evaluation

(either apparent or root cause) would be completed. During the inspection, the team

noted that some CR evaluations were granted multiple time extensions and that other

evaluations were overdue by several months. The team frequently was unable to

determine the basis for the extensions being granted. Additionally, the team noted that,

in some cases, the licensee did not have a documented basis for delaying evaluation of

a discrepant condition until after restart. These issues were discussed with the licensee

for resolution.

Another concern relating to the CAP identified by the team was that the licensee's

electronic system permitted previously approved CRs to be rejected and re-evaluated.

The team was concerned that the process of rejecting a previously reviewed and

accepted evaluation was a potential deficiency in the CAP. The licensee took corrective

actions to discontinue this practice.

The team also noted that, in general, the licensee did not perform extent of condition

reviews and that the few reviews done lacked thoroughness. Revision 4 of the

licensee's CAP procedure called for an assessment of generic implications on those

Enclosure

18

CRs requiring an apparent cause evaluation. The team noted that the lack of such

reviews created the potential for not identifying other problem areas.

Specific examples of the above problems are listed below, and the more significant ones

are discussed in Sections 4OA3(2) and 4OA3(3) of this report.

Root Cause Findings

Root cause for CR 02-06178 didnt contain sufficient information to support

conclusions. It also failed to address three CRs which were rolled into it.

Additionally, the extent of condition review was not well documented (See

Section 4OA3(4)b for details);

Downgrade of SCAQ CRs 02-06356 and 02-06677 were not adequately justified

and, in the case of the first issue, no cause evaluation was performed at all.

(See Section 4OA3(3)b.22 for details);

Root cause was not identified for SCAQ CR 02-04673 because the finding was

historical, also the evaluation failed to identify issues of pre-conditioning and

component limitations (See Section 4OA3(3)b.15 for details);

Apparent Cause Evaluation Findings

Evaluation of the HPI pump minimum flow issue was inadequate (See Section

4OA3(3)b.1 for details);

Evaluation was inadequate in that the consequences of potentially increased

offsite doses due to the degraded condition were not addressed (See

Section 4OA3(3)b.2 for details);

Evaluation failed to address issue identified in the CR (See Section 4OA3(3)b.12

for details);

Evaluation on allowable reactor coolant pump (RCP) stud elongation was flawed

(See Section 4OA3(3)b.19 for details);

Evaluation provided weak basis for not identifying issues (See Section

4OA3(3)b.21 for details);

Evaluation contained incorrect information and inadequately assessed issue

(See Section 4OA3(3)b.20 for details);

Evaluation of the causes for missing or degraded emergency diesel generator

(EDG) tornado missile protection was poor (See Section 4OA3(3)b.23 for

details);

Evaluation for CR 02-05640 was weak and referenced corrective action

documents appeared incorrect;

Enclosure

19

Inadequate evaluation for CR 02-05727;

Inadequate evaluation for CR 02-05738;

Evaluation for CR 02-05885 referenced an incorrect calculation and had a wrong

revision for other another calculation;

Cause analysis for CR 02-06723 did not address that struts were not supposed

to be greased; and

Evaluation did not address temperature increase for CR 02-06893

(Section 4OA5(1)b.2.7).

Extent of Condition Findings

Extent of condition review for CR 02-00412 was inadequate (See

Section 4OA3(2)b.4 for details); and

Required extent of condition reviews for CRs 02-01129 and 02-07188 were not

performed (See Section 4OA3(3)b.7 for details of the latter issue).

At the conclusion of the inspection, the licensee initiated a collective significance review

CR, 03-06908, to address the team's findings regarding CAP deficiencies, especially in

the area of apparent cause evaluations.

.4

Adequacy of Licensee's Efforts to Correct Identified Problems

The team identified examples where inadequate corrective actions were due to the

inadequate cause evaluations. The team also identified examples where corrective

actions were prematurely closed based on unapproved calculations; where actions were

closed without actually completing the work; and where the specified corrective actions

did not resolve the originally identified issue. The team also identified several items

where the corrective actions appeared untimely. Very few effectiveness reviews had

been done at the time of the inspection, so the team was unable to assess the overall

effectiveness of the implemented corrective actions. Most effectiveness reviews for

corrective action items that were implemented via CR 02-00891 had not been completed

by the end of the inspection.

Specific examples of the above problems are listed below, and the more significant ones

are discussed in Sections 4OA3(2) and 4OA3(3) of this report.

A hardware change for CR 02-04680 was indicated as complete when it was not

actually done;

Three examples were identified where the corrective actions were closed before

the calculations were issued (See Sections 4OA3(3)b.17, 4OA3(3)b.19 and

4OA5(1)b.2.23 for details);

Enclosure

20

The diesel driven fire pump heat load was not included in the SW ventilation

system calculation, even though the NRC identified that specific heat load as one

which been missed (See Section 4OA3(3)b.7 for details);

Corrective actions to a Nuclear Quality Assurance (NQA) finding did not address

defined problem - NQA initiated a second CR to address the issue (Section

4OA3(3)b.19);

An NRC identified issue regarding a procedure deficiency was not corrected until

the team questioned the issue (See Section 4OA3(3)b.12 for details);

Corrective action 15 to CR 02-04884 was closed even though not all required

individuals were trained;

Corrective action 30 of SCAQ CR 02-00891 was closed out prior to performing

the required operations confidence reviews.

.5

Review of Engineering Products and Corrective Actions

The team determined that the licensees effectiveness in resolving design deficiencies

was inconsistent. The most difficult area for the licensee appeared to be in regard to

quality of calculations, as many of the calculations reviewed by the team required

multiple iterations to correct team-identified problems. The team attributed this

observation to weak engineering knowledge of the design and licensing basis of the

plant and a lack of attention to detail.

Based on a review of recently approved mechanical engineering design calculations, the

team determined that about 40 percent of the calculations reviewed required generation

of a new CR to fix a calculation problem. Included in the problems were configuration

control issues where design analysis was not controlled. The team also noted use of

non-conservative assumptions, omissions, and errors in recently approved design

calculations.

In the electrical area, the team determined that the electric transient analysis profile

(ETAP) calculations which were completed in 2003, appeared to be well performed.

As a result of the numerous calculational issues identified by the team, the licensee

initiated CR 03-06907 to perform a collective significance review on calculation quality.

Additionally, the licensee initiated CR 03-06909 to perform a collective significance

review of overall engineering design control issues.

Subsequent to the onsite inspection, on November 12 and December 10, 2003, the

licensee presented to the NRC, the planned actions to address the issues and concerns

identified by the CATI. As part of these meetings, the licensee made a number of

commitments to further improve the quality of engineering products such as calculations

and cause analyses. These efforts included expanding the scope of the Engineering

Assessment Board (EAB) reviews to include calculations which supported modifications.

The process improvements were incorporated as part of the licensees Operational

Improvement Plan for Cycle 14, Revision 3.

Enclosure

21

.6

Adequacy of Licensees Efforts to Resolve Procedure Adherence and Quality

Issues

The team noted that there were several programmatic procedural improvements,

including the CAP procedure, the boric acid corrosion control (BACC) program

procedure, and the self-assessment guideline. Additionally, engineering procedures

also improved. Typically, it appeared that the licensee staff did a good job on procedure

development. The team also noted that the licensee identified a number of procedural

adherence problems. The licensee initiated a SCAQ CR in 2002 to evaluate and

address multiple procedure issues.

Many of the teams findings resulted from the licensees failure to adhere to the

corrective action procedure and other procedural requirements. Specific examples of

the above problems are listed below, and the more significant ones are discussed in

Sections 4OA3(2) and 4OA3(3) of this report.

The licensee failed to follow trending and self evaluation procedures and

guidelines (See Section 4OA2(2)b.1).

The licensee's NQA organization identified numerous problems with procedures

(See Section 4OA2(2)b.3 for detail).

(2)

Review of the Licensees Internal Assessment Activities

a.

Inspection Scope

The team examined the licensees program, and implementation thereof, to trend CRs

and analyze the results as delineated in procedures NG-NA-00711, NOBP-LP-2001 and

NOBP-LP-2004. In addition, the team examined the licensees implementation of the

self assessment program. Trending and self assessments were required by the

licensee's procedures. The team also reviewed the licensees implementation of CAP

performance indicators (PIs) to determine their intended use and adequacy in

measuring effectiveness of corrective action implementation. The team also evaluated

the effectiveness of the licensee's internal assessment capability by reviewing selected

NQA audits and available self evaluation reports, which were specifically performed to

assess the implementation of the CAP and which were conducted between January

2002 and August 2003. In addition, the team reviewed the licensees follow-up on

selected NQA findings to determine whether the licensees response was adequate and

timely, and corrective actions were properly prioritized and implemented to prevent

recurrence. The procedure for audit activities performed by the NQA organization was

described in procedure NOP-LP-2004.

b.

Observations and Findings

.1

Trending, Self-Assessment, and Evaluation Program Implementation

Introduction: The team identified that the licensee failed to perform the required CR

trending analysis and to ensure that condition reports were regularly assessed for

indications of adverse trends, generic problems, and repetitive conditions requiring

Enclosure

22

corrective actions. The licensee entered the issue into its corrective action program in

December 2002 and again in July 2003 to re-evaluate the issue, and began the required

trending at the end of the inspection.

Description: The team determined, through reviews of CRs and via interviews that the

licensee had not implemented the CR trending program which was required by

procedure NG-NA-00711. In April 2003, the team determined that trending of

equipment CRs stopped in December 2001, prior to the plant shutting down for refueling

outage (RFO). Departmental and performance improvement group trending activities

stopped in March 2002. This latter cessation was a licensee management decision

because of the number of issues which were being identified during the various

programmatic reviews. However, once the programmatic reviews were completed, the

trending program was not reinitiated in a timely fashion.

Procedure NG-NA-00711 required that CR trending analysis be performed regularly.

Section 6.2 of the procedure stated that the performance improvement manager was to

ensure that CRs were regularly assessed for indications of adverse trends, generic

problems, and repetitive conditions requiring corrective actions. The procedure also

required that indications of potential adverse conditions were to be discussed with

management of the responsible organization to ensure that generic problems, repetitive

conditions or adverse trends were classified as conditions adverse to quality. In

addition, the procedure stated that a quality trend summary was to be prepared at least

quarterly and distributed to managers, directors and the Vice President - Nuclear.

The team determined that a licensee engineer initiated CR 02-10369 on

December 19, 2002, to document that the CR trend analysis had not been reinitiated

even though the discovery phase of the various programmatic reviews was finished.

The CR identified that procedural requirements for trend analysis were not being

followed. The CR also stated that a regular review of CR issues was also required as a

corrective action to a previous audit finding. The licensees evaluation of CR 02-10369

noted that, although the procedurally required trend analysis and trend reporting had not

been resumed, other tasks enacted under the Davis-Besse return to service plan could

have identified generic problems, adverse trends and repetitive conditions. Therefore,

the licensee concluded that no immediate corrective actions were necessary to reinstate

the CR trending program.

The team noted that trend analysis and reporting should contribute to the identification

of potential adverse trends, repetitive conditions, and generic problems before those

trends become significant issues. Programmatic issues were identified by the team

during the inspection, such as inappropriate use of rollovers, calculation problems and

design issues. The team noted that the licensee initiated three condition reports to

evaluate the collective significance of the team's findings.

On July 23, 2003, NQA independently initiated CR 03-05925 which documented

concerns identical to the team's concerns in regard to weaknesses in implementation of

trending and non-compliance with trending requirements. NQA identified that, in most

organizations, activity codes and trend codes were not routinely trended or analyzed and

that management involvement with trending, in some organizations, was minimal or

nonexistent.

Enclosure

23

The team determined that the framework for an effective trending program existed, but it

was not being implemented and that management attention and focus was needed in

order to ensure that the programs were reinstated. Due to the team identifying potential

trends in several areas, the team was unable to confirm the licensees position that

reliance on processes developed for the extended shutdown could substitute for the

trending analysis process. The licensee entered the issue into its corrective action

program in December 2002 and again in July 2003 to re-assess the issue, and re-

instituted the required trending at the end of the inspection.

The team also assessed the licensees self assessment program implementation. The

need for a self assessment and evaluation program was delineated in NOBP-LP-2001,

NOBP-LP-2004, and the Davis-Besse self evaluation process guide. The purpose of

these self assessment and evaluation guidelines was to continue plant improvement

through implementation of learning organization behaviors by the Davis-Besse

management team to periodically critically assess organizational performance against

established standards/expectations of performance and industry-best practices. The

self evaluation was intended to identify organizational strengths, weaknesses,

challenges, and areas of improvements.

The self evaluation process guideline stated that each quarter, the section managers

and directors were to present the results from their self-evaluations to the Davis-Besse

Vice President. In April 2003, the team noted that the licensee stopped performing the

required self evaluations by the different plant departments after the first quarter in

2002. In July 2003, NQA identified in CR 03-05925 that most site organizations were

not actively performing self-evaluations. The licensee was in the process of replacing

the guideline and reinstating the self-evaluations at the end of the inspection.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to perform the required CR trending. Since there was a performance

deficiency, the team compared this performance deficiency to the minor questions

contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports." The team concluded that the issue was minor because the lack of CR

trending occurred while the unit was shutdown.

Enforcement: The failure to perform CR trending and department self evaluations from

March 2002 until the end of the CATI on-site inspection in September 2003, constitutes

a violation of 10 CFR Appendix B, Criterion V, which has minor significance and is not

subject to enforcement action in accordance with Section IV of the NRCs Enforcement

Policy.

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case based on the length of time

the licensee was not in compliance.

.2

Corrective Action Program Performance Indicators

During the period when the licensee was not performing trending or self-evaluations, PIs

on the restart performance and CAP effectiveness were published weekly. The CAP

effectiveness PIs included corrective action effectiveness, CR category accuracy, CR

evaluations, corrective action resolution, CR self identification, and management

Enclosure

24

observations. Restart PIs relating to CAP implementation included CR evaluations, CR

resolution, root cause evaluation quality, program and process error rate, CR category

accuracy, CR operations review, corrective action resolution and CR self-identified rate.

The team noted that the indicators generally showed improving trends and that, in most

cases, the licensee was meeting established goals. Action plans were in place for those

PIs which were not meeting their goal in order to improve performance prior to restart.

The team reviewed these PIs and determined that the PIs generally reflected CAP

performance. The team noted that, for example, PI P-01, "Corrective Action Program

Implementation," rated CAP implementation from January to September 2003 as Red

for six of the nine months and as Yellow for the remaining three months. During the

review of P-01, the team noted that the licensee has routinely determined that the

"Repeat Events" element was Green. This meant that there were no repeat SCAQ

events in the last two years. The team determined that, in 2002, the licensee initiated

six SCAQ CRs for what appeared to be a recurring trend of untimely and ineffective

CAP resolution and program implementation. These included CRs 02-02419, 02-02584,

02-03497, 02-03674, 02-04884 and 02-07328. The licensee stated that the above

SCAQ CRs could not be considered repeat events because the events did not involve

similar tasks, causes and consequences. Based on the licensees definition, SCAQ

CRs had to be identical in all three (tasks, causes and consequences) as well as

occurring within two years of each other in order for them to be considered as a repeat

event. The team considered the licensees definition to be limiting, as the above CRs

appeared to the team to document repeat events and an adverse trends. The team also

noted that, because the licensee limited the definition of repeat events to SCAQ CRs,

low level issues that were occurring on a repeat basis (such as repeat CRs) did not

show up in the PI.

The team noted that the PIs did not always provide an accurate indication of the health

of the CAP implementation. For example, the team identified a number of examples

where CRs were indicated as closed in the system when, in reality, the issues were

transferred to other CRs and may not have been either evaluated or corrected.

Finally, the team noted that the PI which assessed quality of engineering products had

shown a negative trend for five weeks from the end of July to the beginning of August

2003. Despite the negative trend, the indicator stated that engineering product quality

had significantly improved since initiation of the EAB. The team questioned the licensee

as to the positive statement on the trend report when the graph had been showing a

declining trend in quality of engineering products. After questioning by the team, the

licensee examined additional engineering products and informed the team that the

products had improved and the latest trend information reflected that improvement.

.3

Nuclear Quality Assessment Audits and Self Assessments of Corrective Action

Program Implementation

The NQA organization conducted various performance-based and program-based

audits of the CAP and its implementation. Some audits evaluated specific activities,

while other audits were broad evaluations of processes or department performance.

Generally, the team found NQA audits to be of a critical nature and to adequately

Enclosure

25

identify CAP implementation deficiencies. The NQA auditors identified conditions

adverse to quality which were documented on CRs and tracked in the CR database.

NQA used the following performance categories to rate effectiveness of the

implementation of CAP: Good Performance, Satisfactory Performance, Marginal

Performance and Unacceptable Performance. The table below documents the results

of the six NQA audits reviewed by the team:

NQA Rating of Corrective Action Program Implementation

Report Number

Date Completed

Primary Rating

Elements Rating

DB-C-02-02

August 9, 2002

Marginal

Unacceptable

DB-C-02-03

November 14, 2002

Marginal

Unacceptable

DB-C-02-04

February 19, 2003

Not Rated

Marginal

DB-C-03-01

May 28, 2003

Not Rated

Marginal

DB-C-03-02

September 1, 2003

Satisfactory1

Not Rated

DB-C-03-03

November 17, 2003

Marginal

Not Rated

1Note: The "satisfactory" rating was for the overall CAP and did not focus on

implementation.

The team noted that the selected CAP implementation areas assessed by NQA from

March 2002 to October 2003 were rated as either "marginal" or "unacceptable." For

example, a NQA CAP focused assessment was conducted between April 4 through

July 4, 2003, and identified CAP and implementation deficiencies which were similar to

those identified by the NRC CATI (NQA initiated 24 CRs). Examples included: lack of

trending activities to identify adverse to quality conditions, use of PI to assess CAP, less

than adequate cause evaluations, corrective action item implementation timeliness, poor

documentation of corrective actions, inadequate peer reviews, lack of rigor,

configuration control issues, rollovers concerns, and failure to comply with administrative

requirements of the NOP (mostly by engineering). Similar findings were noted during

the November 2003 NQA audit.

Overall, the team concluded that NQA was performing sufficiently probing assessments

of the licensees corrective action program implementation.

(3)

Management CAP Meetings

a.

Inspection Scope

One of the key building blocks in the licensees return to service plan was the

management and human performance excellence plan. The purpose of this plan was to

address the fact that, "management ineffectively implemented processes, and thus

Enclosure

26

failed to detect and address plant problems as opportunities arose." One of the primary

management contributors to this failure was the ineffective implementation of the CAP.

During this inspection, the team attended and assessed the licensee management

activities and involvement in selected corrective action related meetings. During these

meetings the licensee conducted a review and classification of CRs, evaluated and

performed a critique of root cause and engineering products, prioritized work activities,

and provided work completion schedule extensions for ongoing work activities. The

team attended and observed various corrective action management oversite meetings

including the corrective action review board (CARB), the restart station review board

(RSRB), and the management review board (MRB).

b.

Observations and Findings

Corrective Action Review Board Meetings: The purpose of the meetings was to

evaluate completed root causes performed to identify and address causes of more

significant plant related issues which were documented in CRs. The team concluded

that the CARB was comprised of experienced individuals with a wide range of

knowledge. The CARB was primarily involved in reviewing the cause analysis packages

for completeness and adequacy of technical information. The CARB also concentrated

on potential design and safety issues and ensured that the engineering

recommendations for resolution of the identified issues appeared adequate to address

the causes.

Restart Station Review Board: One of the purposes of the RSRB was to screen and

classify CRs as to whether they needed to be addressed prior to restart. The team

noted that CRs were screened and classified into one of four categories based on

whether the corrective actions: (1) were necessary to address NRC Manual Chapter

(MC) 0350, "Oversight of Operating Reactor Facilities in an Extended Shutdown as a

Result of Significant Performance Problems" issues; (2) were necessary to address

Davis-Besse restart expectations; (3) could be implemented following plant restart; or

(4) could be addressed at a time unrelated to plant restart. Once the licensee staff

developed corrective actions to address the issues documented in the CRs, the RSRB

also screened the proposed corrective actions to ensure that the underlying issues were

fully addressed. The team observed RSRB members interactions and noted good

questioning attitude and generally appropriate classification of CRs.

Management Review Board: During the MRB meetings, the licensee discussed

corrective action items including review of latest initiated CRs and the potential for

indications of adverse trends. Management appeared to be engaged in the CAP during

these meetings.

Three Day Look-Ahead Committee: This committee discussed CR status and due

dates. The team attended several meetings at the beginning of the inspection and

noted that many due dates were being extended without formal justification or

documented management approval. After the team commented on this practice, the

licensee no longer allowed informal extensions.

Enclosure

27

The team concluded that the management meetings and processes had an appropriate

approach for evaluating and characterizing newly identified issues. The members

appeared to be qualified and knowledgeable of the requirements.

4OA3 Event Response Follow-up - Special Inspection (71153 and 93812)

(1)

Background

Davis-Besse CAP Compliance Review

As part of the licensees restart action plan to identify, monitor and complete all actions

necessary for safe and reliable return to service the licensee initiated various teams

which were tasked with reviewing selected plant programs to ensure that the programs

were fulfilling required obligations and were acceptable to support plant restart. The

CAP was selected as one of the plant programs to receive a comprehensive Phase 2

review as described in the Davis-Besse program compliance plan and procedure

NG-EN-00385.

The review was conducted between June 10 and August 9, 2002. Results were

documented in the "Corrective Action Program Review" report and included numerous

concerns relative to the CAP process and implementation. The Phase 2 review team

determined that the CAP generally met regulatory requirements and that the identified

problems were primarily associated with program implementation. However, the review

team also concluded that the CAP was not consistently implemented in full compliance

with the spirit and letter of the governing and implementing documents and that the CAP

needed to be strengthened prior to restart of the plant.

The primary problem identified during this review was summarized as, "inadequate

implementation of the CAP." Examples of ineffective CAP implementation issues

identified as a result of this review included: (1) a reluctance to identify conditions

adverse to quality relating to organizational, human performance and programs in a CR;

(2) a recurring trend of inadequate CR cause evaluations and corrective actions; (3) a

recurring trend of inadequate, untimely, ineffective and improperly closed corrective

actions; (4) MRB deficiencies; (5) a need for improvement in the trending program; (6)

untimely resolution of issues and supervisory and senior reactor operator reviews; (7)

ineffective corrective action to preclude repetition; and (8) recurring trend of procedure

non-compliance. These and other findings were determined to be consistent with the

root cause analysis reports for CR 02-00891.

To resolve the identified deficiencies and to improve program implementation, the

licensee generated numerous CRs that included recommended corrective actions to

resolve and correct the noted deficiencies. The majority of the CRs from the review

were classified as requiring evaluation and resolution prior to restart, although some

were classified as post restart. Many of the corrective action items were rolled into

CR 02-04884. As part of the corrective actions to address these findings the licensee

determined that training of staff and changes to the program documents were necessary

in order to restore an effective CAP.

Enclosure

28

Assessment of the Corrective Action Program Compliance Review

The CATI team reviewed selected corrective actions to determine the effectiveness of

the licensees implementation of the specified corrective actions. The team determined

the licensees Phase 2 review of the CAP was comprehensive and in accordance with

procedure NG-EN-00385. The team concluded that the CAP appeared to contain many

of the programmatic elements needed for a successful program; however, station

personnel did not consistently identify or effectively resolve plant issues. This was

demonstrated by the team identifying many of the same issues as those identified in the

Phase 2 review.

(2)

Detailed Team Review of Licensee Corrective Actions Implemented to Address

Electrical Issues Previously Identified by NRC or the Licensee

a.

Inspection Scope

The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,

and resolve the identified equipment, human performance and/or programmatic adverse

to quality plant conditions. The team mainly focused on plant systems design and

licensing basis requirements issues which were previously identified by the NRC, the

licensee and others during various design reviews conducted in 2002. The team

assessed effectiveness of the licensees corrective actions implemented to address

previously identified electrical engineering design issues.

b.

Observations and Findings

.1

Undervoltage Time Delay Relay Setting Did Not Account For Instrument

Uncertainties

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

"Design Control," having very low safety significance (Green). Specifically, the licensee

failed to translate instrument uncertainties into the undervoltage time delay setting

specification for the 4160 Vac buses C1 and D1. Following discovery, the licensee

re-evaluated the potential temperature effects to the time delay relays.

Description: The licensee identified in CR 02-05632 that the time delay relays for the

59 percent undervoltage condition on 4160 Vac buses C1 and D1 may not have met the

allowable value of 0.5 +/- 0.1 seconds contained in technical specification (TS )

Table 3.3-4 because instrument uncertainties were not included. The licensee later

initiated CR 03-01448 to specifically determine if the TS value had been exceeded in the

past. The licensee determined that the primary cause for fluctuations in the time delays

were temperature variations in the room where the relays were located. The licensee

determined that during periods of cool weather, the room would maintain a temperature

of approximately 70 degrees Fahrenheit (F), because the fans in the room would

recirculate air from the turbine building to warm the switchgear room when the fan outlet

temperature dropped below 70F. However, the licensee stated that, during the

summer, the effects on the time delay relays would be insignificant. Specifically,

CR 03-01448 stated, "Only during summer does the room temperatures increase, and

even then it does not typically vary during the day. . . Based upon the operation of the

Enclosure

29

ventilation system, there is very little potential for the relays to experience a significant

temperature rise between the monthly tests."

The team questioned this logic, because it was not apparent that temperature effects,

particularly in the summer when outside temperatures could regularly exceed 90F,

would not affect the time delay relays, especially when past experience, which showed

that some room temperatures could exceed 120F on hot days, was considered. Based

upon the team questions, the licensee re-evaluated the potential temperature effects to

the time delay relays. After performing additional calculations, the licensee determined

that increased temperature could cause the time delay to operate outside of its TS

limits. Also, the licensee determined that in the past, there was at least one occasion

where the temperature in the room was so high that the time delay could have been

outside of its TS allowed value. The team was informed by the licensee that, even if the

allowable value requirement had been exceeded, the additional time delay would have

had negligible effect on the capability to achieve timely emergency core cooling system

(ECCS). As the licensee concluded that the relay would have been able to function

even though it did not meet its TS allowable value, the licensee did not consider the

relay to have been inoperable. The team did not independently verify this conclusion.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to translate instrument uncertainty into the specification for undervoltage

time delay relays for the 4160 Vac buses C1 and D1. Since there was a performance

deficiency, the team compared this performance deficiency to the minor questions

contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports." The team concluded that the issue was more than minor because this was a

design issue which affected the mitigating system cornerstone. The licensee had to

perform calculations to show that the relays were within the TS allowable values and the

licensee determined that the increased temperature could cause the time delay to

operate outside of TS limits. Although the licensee acknowledged that there had been

at least one occasion where inclusion of instrument uncertainties into the allowable

value would have resulted in an instrument being technically inoperable, the licensee

believed the instrument would still have performed its safety function. Therefore, the

licensee did not consider the instrument to have been inoperable. The team reviewed

this finding in accordance with IMC 0609, "Significance Determination Process, and

answered no to all five screening questions in the Phase 1 Screening Worksheet

under the Mitigating Systems column. The team concluded the issue was of very low

safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to assure that the regulatory requirements and

the design basis of the plant were accurately translated into specifications. Specifically,

the instrument uncertainty was not translated into specification for the undervoltage time

Enclosure

30

delay relays for the C1 and D1 4160 Vac buses. The licensee had previously entered

the issue into its CAP as CRs 02-05632 and 03-01448. Because this violation was of

very low safety significance and because it was entered into the licensees CAP, this

violation is being treated as a NCV, consistent with Section VI.A of the NRC

Enforcement Policy. (NCV 05000346/2003010-03)

.2

Lack of 480 Vac Class 1E Motor Thermal Overload Protection

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to provide

motor thermal overload protection for the Class 1E 480 Vac distribution system.

Following discovery, the licensee physically modified approximately 53 thermal overload

circuits to resolve the discrepancy. The primary cause of this violation was related to

the cross-cutting area of human performance because the licensee did not identify the

lack of thermal overload protection was an unanalyzed condition and that the station

was not in compliance with the updated safety analysis report until identified by the

team.

Description: The team reviewed the design criteria manual for the 480 Vac distribution

system. Section 5.4.3.2, "460V Motors Fed from Motor Control Centers," of this design

criteria stated that, "Starters should be equipped with overload relays to provide motor

overload protection. For Class 1E motor operated valves, dampers, pumps, and fans,

the thermal overload relays should be bypassed to avoid tripping during emergency

conditions." This design criteria contradicted Updated Safety Analysis Report (USAR)

Section 8.3.1.2.11, "Protection Systems," which stated, "Protection systems are

provided and designed to initiate automatically the operation of the appropriate

equipment. Necessary protective devices are provided to isolate failed equipment and

to identify the equipment that has failed. For the protection system related to

engineered safety features and essential functions, complete redundancy,

independence, and inservice testability is maintained."

The team determined that as a consequence of following the design criteria manual

guidance, the licensee had failed to ensure that the 480V Class 1E circuits were

designed so that the protection systems would automatically initiate appropriate

equipment, including motor operated valves, dampers, pumps, and fans, as required by

the USAR.

The team asked the licensee to provide verification that each circuit fed by a Class 1E

480V motor control center which had its overload protection bypassed or inactivated

would be capable of carrying overloads ranging from full load amperes to locked rotor

amperes on a continuous basis, or until interrupted, without exceeding the ratings of the

circuit breaker, the contactor, the bypassed overload device, or the cable. The team

also asked the licensee to assure that when overload protection was bypassed, it did not

result in jeopardizing the safety function, or in degrading other safety systems.

As a result of the team's questioning, the licensee identified that, despite the numerous

programmatic design reviews that were completed, engineering had not identified this

discrepancy and there were many circuits where completion of the safety function could

not be demonstrated due to bypassing the thermal overload protection. An overload

Enclosure

31

condition in a single circuit could result in opening of the upstream circuit breaker to the

bus, thus removing 480V power to all other Class 1E equipment connected to that bus.

The team also identified additional bypassing of thermal overload protection on Class 1E

480V loads, where the design criteria did not allow such bypassing.

The licensee characterized this issue as having "potential for a significant impact on

safety" and wrote numerous CRs to address the issue. Subsequently, the licensee

modified approximately 53 thermal overload circuits as part of the issue resolution.

There was reasonable assurance that the condition did not result in a loss of system

function

During review of this issue, the team also noted an example of an ineffective roll-over in

that some of the concerns identified in CR 03-02616 were rolled over to CR 03-03572

and were not adequately addressed. The team was concerned about this issue

because it had occurred after the licensee had revised its roll-over process to address

concerns expressed by the team earlier in the inspection.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to provide protective devices, such as thermal overloads, for 480V Class

1E circuits as specified in design documents. Since there was a performance

deficiency, the team compared this performance deficiency to the minor questions

contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports." The team concluded that the issue was more than minor because this was a

design issue which affected the mitigating systems cornerstone. The licensee failed to

ensure that bypassing the thermal overload protection would result in completion of

safety functions and subsequently had to install thermal overload protection in order to

meet the design requirements. The team reviewed this finding in accordance with IMC

0609, "Significance Determination Process, and answered no to all five screening

questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.

The team concluded the issue was of very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis are correctly translated into specifications, drawings, procedures, and

instructions. USAR Section 8.3.1.2.11, "Protection Systems," stated, in part, that,

protective devices are provided to isolate failed equipment and to identify the equipment

that has failed. Furthermore, for the protection system related to engineered safety

features and essential functions, complete redundancy, independence, and inservice

testability is maintained.

Contrary to the above, the licensee failed to correctly translate the design basis into

specifications. Specifically, the licensee failed to provide the necessary protective

devices, such as thermal overload protection for the for 480V Class 1E circuits. The

protection was required to isolate failed equipment and limit fault propagation. The

licensee entered the issue into its CAP as CRs 03-02597, 03-02616, 03-03572,

03-04264, 03-04303, 03-04375, 03-06475, 03-06567 and 03-07031. Because this

violation was of very low safety significance and because it was entered into the

licensees CAP, the violation is being treated as a NCV, consistent with Section VI.A of

the NRC Enforcement Policy. (NCV 05000346/2003010-04)

Enclosure

32

.3

Failure to Perform Direct Current Contactor Testing to Ensure Minimum Voltage

at Motor Operated Valves

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,

Test Control, having very low safety significance (Green). Specifically, the licensee

failed to adequately test direct current (DC) contactors related to two safety related

motor operated steam valves associated with the AFW system. Following discovery, the

licensee entered the issue into the corrective action program and was re-evaluating the

basis for acceptability of these valves. The primary cause of this violation was related to

the cross-cutting area of problem identification and resolution because, although the

issue was identified in 2002, the licensee did not take corrective action until prompted by

the team in 2003.

Description: The team reviewed CR 01-03059,which documented the issue of minimum

voltage available at two safety related motor operated steam valves associated with the

AFW system. One of the valves was normally closed and was required to be opened

under certain conditions to allow the AFW system to perform its intended function. It

had a cable conductor circuit length of 6,814 feet for the automatic opening function.

The licensees corrective action to the issue was to revise calculation C-EE-002.02-010

to include the valves which had not been previously addressed in the calculation. This

corrective action was implemented in April 2002. In review of the calculation, the team

noted that Attachment 27 of the calculation included the test data used to establish a

minimum voltage for the DC contactors. The team ascertained that the testing was

based on a single device and lacked sufficient basis to conclude that other contactors

would actuate under similar conditions. In addition, the test used an uncalibrated meter

to collect data. The team also noted that no adjustment had been made to factor plant

environmental conditions into the results. The licensee issued CR 03-07069 during the

inspection to document this deficiency in testing methodology.

As a result of the deficiencies in the testing methodology, the team could not conclude

that the valves had sufficient minimum voltage at the component to perform their safety

function. The team also noted that the licensee's evaluation of the team-identified

deficiency was that it was acceptable because of the single failure criteria (i.e., that even

if one valve failed, the other train would be available because the single failure had

already occurred). The team informed the licensee that this appeared to be an

inappropriate application of the single failure criteria.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to ensure proper testing of DC contactors. Since there was a

performance deficiency, the team compared this performance deficiency to the minor

questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor

Inspection Reports." The team concluded that the issue was more than minor because

the licensee had relied upon an inadequate test to demonstrate that the contactors were

qualified to perform under required conditions and because the contactors were installed

in the plant during previous operating cycles. The licensee determined that the valves

had always been operable. This was a design qualification issue which affected the

mitigating systems cornerstone. The team reviewed this finding in accordance with IMC

0609, "Significance Determination Process, and answered no to all five screening

Enclosure

33

questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.

The team concluded the issue was of very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI requires, in part, that a test

program shall be established to assure that all testing required to demonstrate that

structures, systems, and components will perform satisfactorily in service is identified

and performed in accordance with written procedures. Test procedures shall include

provisions for assuring that all prerequisites for the given test have been met, that

adequate test instrumentation is available and used, and that the test is performed

under suitable environmental conditions.

Contrary to the above, during the testing for establishing a minimum voltage for DC

contactors, the licensee failed to: ensure the components would perform satisfactorily in

service; failed to use adequate test instrumentation; and failed to ensure the test was

performed under suitable environmental conditions. Specifically, the licensee used a

sample size of one DC contactor to justify pick-up voltages of other DC contactors in the

plant. In addition, the licensee used uncalibrated instrumentation and failed to consider

actual plant environment to which the DC contactors would be subject.

The licensee entered the issue into its CAP as CR 03-07069. Because this violation

was of very low safety significance and because it was entered into the licensees CAP,

the violation is being treated as a NCV, consistent with Section VI.A of the NRC

Enforcement Policy. (NCV 05000346/2003010-05)

.4

Failure to Verify Adequacy of Short Circuit Protection for Direct Current Circuits

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,

"Corrective Action," having very low safety significance (Green). Specifically, the

licensee failed to identify and correct inadequate short circuit protection for DC circuits.

Following discovery, the licensee issued Condition Report 03-06944 to document the

deficient circuit protection for valves having extremely long circuit lengths. The primary

cause of this violation was related to the cross-cutting area of problem identification and

resolution because the licensee had missed several opportunities to identify it as part of

corrective actions for previously identified DC circuit deficiencies.

Description: While reviewing CRs 01-03059 and 02-00412 and calculation

C-EE-002.01-010, the team questioned the adequacy of DC circuit protection for long

DC circuits, such as the one described in Section 4OA3(2)b.3, which had a cable

conductor circuit length of 6,814 feet. Subsequently, the licensee evaluated the

adequacy of the fuse sizing and identified that, in the case of short circuits, the circuit

resistance could be high enough to preclude operation of the fuses protecting circuit,

i.e., the fuses protecting the circuits were oversized for the application. Thus, a short

circuit current could be allowed to flow for an indeterminate length of time. The short

circuit current would only be interrupted after considerable damage had been made to

safety related equipment and could result in damaging fires which could affect

redundant safety related trains. The licensee issued CR 03-06944 to document the

deficient circuit protection for valves having extremely long circuit lengths. Subsequent

to the inspection, the licensee developed an engineering package to replace the fuses in

March 2004. The inspectors reviewed the licensees engineering package and

Enclosure

34

concluded that the projected completion date appears reasonable and commensurate

with the safety significance of the issue.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to verify the adequacy of short circuit protection for DC circuits. Since

there was a performance deficiency, the team compared this performance deficiency to

the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power

Reactor Inspection Reports." The team concluded that the issue was more than minor

because the licensee had to perform calculations to determine if the fuses would

adequately protect the equipment and because modifications to those fuses were

required. This was a design issue which affected the mitigating systems cornerstone.

The team reviewed this finding in accordance with IMC 0609, "Significance Determination

Process, and answered no to all five screening questions in the Phase 1 Screening

Worksheet under the Mitigating Systems column. The team concluded the issue was of

very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI requires, in part, that

conditions adverse to quality be promptly identified and corrected.

Contrary to the above, as of August 25, 2003, the licensee did not promptly identify and

correct a condition adverse to quality in that DC circuits were not adequately protected

against short circuits, a condition adverse to quality. Specifically, the licensee missed

several opportunities in 2001 and 2002 to identify that there was no basis ensuring

adequate short circuit protection for DC circuits and did not initiate corrective actions to

ensure that fuse sizing was adequate for long DC circuits such as those for motor

operated valves MV0106 and MV3870. The licensee entered this issue into its

corrective action as CR 03-06944. Because this violation was of very low safety

significance and because it was entered into the licensees CAP, this violation is being

treated as a NCV, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000346/2003010-06)

.5

Lack of Calculations to Ensure Minimum Voltage Availability at Device Terminals

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to confirm

operability of DC contactors by ensuring that minimum voltage was available at the

safety related device terminals. The licensee missed several opportunities to correct

this design deficiency. Following discovery, the licensee issued Condition Report

03-06956 and evaluated the issue. The primary cause of this violation was related to

the cross-cutting area of problem identification and resolution because, although the

issue was identified in 2002, the licensee failed to take appropriate corrective action to

thoroughly evaluate the problem until prompted by the team in 2003.

Description: As a part of CR 01-03059, the licensee performed an extent of condition

evaluation and identified that the DC voltages in calculation C-EE-002.01-010 evaluated

available voltage to the panel terminals only. The calculation did not confirm sufficient

voltage at device terminal for proper operation. The licensee issued CR 02-00412 to

document this deficiency. In response to this CR, the licensee issued a revision to the

calculation.

Enclosure

35

During review of calculation C-EE-002.01-010, the team determined that the lowest

voltage was 106.38V, which would occur during the first one minute discharge period.

The calculation was potentially non-conservative because it failed to address resistance

of contacts and fuses which would contribute to additional voltage drop in the circuits.

Conservatism existed in the calculation since all loads were assumed to run

continuously and simultaneously during the first minute of battery discharge. Additional

conservatism was identified during service testing of the battery with the plant

anticipated loads. Nevertheless, the team could not conclude that the conservatism was

sufficient to bound the undetermined voltage drop in part of the circuits. Therefore, it

was not known whether the device terminal voltage present under the design basis

conditions would be sufficient to ensure proper operation of safety related devices.

Upon determination that the actual voltage at the devices had not been evaluated in the

calculation, the licensee identified a potential SCAQ because potential operability

concerns were raised that could have affected numerous pieces of safety related

equipment, the licensee did not take actions to ensure operability. Specifically, the

licensee did not have a documented basis for resolving the operability concern for

equipment which might not have sufficient voltages to ensure proper operation. The CR

stated that, "preliminary reviews indicate that there are no operability concerns" and the

due date for the corrective action to evaluate the loads connected to the panels was

assigned as a post-restart action. After the operability issue was raised by the team, the

licensee issued CR 03-06956 for the lack of basis for deferring corrective action. The

licensee performed additional analysis and extent of condition reviews. The licensee

determined that there were no operability issues based on the results of the re-analysis.

The team reviewed these re-analyses and concluded there is reasonable assurance that

the affected components are operable.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to ensure the availability of minimum voltage at the safety related device

terminals. Specifically, the licensee had not performed design analyses or calculations

to demonstrate that end devices would have sufficient voltage available to perform the

design function. Since there was a performance deficiency, the team compared this

performance deficiency to the minor questions contained in Appendix B, "Issue

Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded

that the issue was more than minor because the licensee had to perform calculations to

demonstrate that the devices had sufficient voltage to perform their safety function.

Based on the evaluation performed as a corrective action to CR 03-06956, the team had

reasonable assurance that affected components were operable. This was a design

issue which affected the mitigating systems cornerstone. The team reviewed this

finding in accordance with IMC 0609, "Significance Determination Process, and

answered no to all five screening questions in the Phase 1 Screening Worksheet

under the Mitigating Systems column. The team concluded the issue was of very low

safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis are correctly translated into specifications, drawings, procedures, and

instructions. measures be established to assure that applicable regulatory requirements

and the design basis were correctly translated into specifications, drawings, procedures,

Enclosure

36

and instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee had failed to ensure that minimum voltage would be

available at the safety related device terminals. The calculation performed by the

licensee did not confirm that sufficient voltage would exist at the device terminals for

proper operation of safety related components during design basis events. The licensee

issued CR 03-06956 to address this deficiency. Because this violation was of very low

safety significance and because it was entered into the licensees CAP, this violation is

being treated as a NCV consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000346/2003010-07)

.6

Raychem' Splice Removal on Containment Air Cooler Motor Cables

Introduction: The team identified a performance deficiency involving the failure to

properly remove Raychem' splices during the CACs motor replacement. Following

discovery, the licensee entered the issue into its corrective action process. After NRC

identified the cause of the condition, the licensee took corrective actions. This was a

minor violation.

Description: During CAC motor replacement, the licensee identified splitting of the

motor cable insulation as documented in CR 02-05459. The cable jacket and insulation

to the three CAC motor high speed windings were found to be split at the ends which

were normally covered by Raychem' heat shrink sleeves. The damage was observed

after the Raychem' sleeves were removed for de-terminating the motors. In 2002, the

NRC examined this issue and concluded that the CAC cable had apparently been cut by

a sharp instrument, rather than the result of an aging or contamination related

mechanism as initially assumed by the licensee. The NRC determined that the splitting

was in fact a deep gash and the licensee subsequently determined the gash was

inflicted by a contractor when removing the Raychem' sleeves with a knife. To

address this concern, the licensee initiated work orders to replace the section of the high

speed cable of the three CAC motors between the motor and the penetrations with an

equivalent cable. The work procedures were revised, and the workers received training

on the revised procedures.

The approved method for removal of Raychem' sleeves was prescribed in

maintenance procedure DB-ME-09500, "Installation and Termination of Electrical

Cables," which required that Raychem' sleeves be removed by lightly scoring the

sleeve with a knife and then applying heat to remove the sleeve. During the licensee

investigation of the issue, the contractor performing this activity stated that he was not

trained on the Raychem' removal technique and was not aware of the applicable

procedure. However, the licensees cause analysis determined that the contractor

performing the task had been trained and qualified. Nevertheless, the contractor did not

perform the Raychem' sleeve removal in accordance with appropriate and applicable

procedures. At the time of the inspection, the team noted that the licensee had not

documented whether an extent-of-condition review was performed to determine if other

maintenance activities were incorrectly performed. On March 2, 2004, the licensee

Enclosure

37

informed the team that the individual had not removed any other Raychem' splices in

the past and the subject work activity was limited to this individual only.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to follow the maintenance procedure for removing Raychem' sleeves.

Since there was a performance deficiency, the team compared this performance

deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC

0612, "Power Reactor Inspection Reports." The team concluded that the issue was

minor because it was identified while the system was out of service, and it was corrected

before the system was returned to service.

Enforcement: The failure to follow the maintenance procedure for removing Raychem'

sleeves constituted a violation of 10 CFR Appendix B, Criterion V, which has minor

significance and is not subject to enforcement action in accordance with Section IV of

the NRCs Enforcement Policy. The licensee entered the issue into its CAP as

CR 02-05459.

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case since the licensee had not

documented whether any extent-of-condition review had been performed and the

underlying cause is similar to that of other findings in this report.

.7

Review of Calculation on the Electric Transient Analysis Profile

Introduction: The team reviewed ETAP calculation C-EE-015.03-008, Revision 2, to

evaluate technical adequacy.

Description: A third revision to the calculation was under way during the inspection and

was not scheduled to be completed until after the inspection was over. The fact that the

licensee was continuing to revise the calculation hampered the team's overall ability to

assess its acceptability. However, the calculation appeared to be generally well

performed and did successfully resolve a multitude of issues. The licensee also

performed a very good self-assessment with an industry group comprised of outside

independent consultants. However, the team considered the ETAP calculation

development to be very slow in regards to implementation of corrective actions. For

example, changes in auto transfer functions and the EDG calculation which were

completed in January 2003 had not yet been incorporated into the main ETAP

calculation. The team also observed that the calculation was performed by contractors

and that the licensee's internal knowledge of the calculation appeared limited.

Analysis: As a minor issue, the team noted that procedure NOP-CC-3002 required that

calculations be entered into the calculation database prior to issuing of a new revision.

However, the team identified that document control was not notified upon issuance of a

new revision to calculation C-EE-015.03-008 (Revision 2).

Enforcement: The failure to enter the revision of a procedure into the database prior to

its issuance constitutes a violation of minor significance that is not subject to

enforcement action in accordance with Section IV of the NRCs Enforcement Policy.

The licensee documented the issue in CR 03-06989.

Enclosure

38

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case it represented an example

of calculation weakness and the underlying cause is similar to that of other findings in

this report.

.8

Inadequate Grid Voltage Calculations

Introduction: The team identified that the licensee failed to consider the worst case grid

voltages in the short circuit analyses. Following discovery, the licensee entered the

issue into their corrective action program and performed new calculations to address the

issue.

Description: The licensee initiated CR 02-06302 to document that the licensee had not

considered the worst case grid voltage. This CR described the issue as being

administrative in nature and having no effect on the results. This conclusion was

incorrect and was so recognized in CR 02-06837.

The team ascertained that the maximum grid voltage was an important parameter which

affected the accuracy of the short circuit calculations. The postulated short circuit

current would proportionally increase for higher grid voltage, therefore, calculations

performed for lower grid voltages would be non-conservative. The team reviewed this

item and determined that calculation C-EE-015.03-003 was superseded with calculation

C-EE-015.03-008, which utilized the ETAP program described in Section 4OA3(2)b.7.

The new calculation had taken into account the worst grid voltage conditions.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to analyze the grid voltage under worst case design conditions. Since

there was a performance deficiency, the team compared this performance deficiency to

the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power

Reactor Inspection Reports." The team concluded that the issue was minor because

although the licensee had to perform calculations, the new calculation had taken into

account the worst grid voltage conditions and the results were acceptable.

Enforcement: The failure to translate the worst case grid voltage into calculations of

record constituted a violation of 10 CFR Appendix B, Criterion III, which has minor

significance and is not subject to enforcement action in accordance with Section IV of

the NRCs Enforcement Policy. The licensee entered the issue into its CAP as

CRs 02-06302 and 02-06837.

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case it represented an example

of calculation weakness and the underlying cause is similar to that of other findings in

this report.

Enclosure

39

(3)

Detailed Team Review of Licensee Corrective Actions Implemented to Address

Mechanical Issues Previously Identified by NRC or the Licensee

a.

Inspection Scope

The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,

and resolve the identified equipment, human performance or programmatic adverse to

quality plant conditions. The team mainly focused on plant systems design and

licensing basis requirements issues which were previously identified by the NRC, the

licensee and others during various design reviews conducted in 2002. The team

assessed effectiveness of the licensees corrective actions implemented to address

previously identified mechanical engineering design issues.

b.

Observations and Findings

.1

High Pressure Injection Pump Operation Under Long Term Minimum Flow

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to verify

that the HPI pumps could operate under design basis minimum flow requirements since

initial plant startup. Following discovery that the design basis minimum flow

requirements were significantly below industry standards, the licensee entered the issue

into its corrective action program, performed a test which demonstrated satisfactory

pump operation for an extended period of time at a higher flow rate, and began the

steps to change the design basis minimum requirement. The primary cause of this

violation was related to the cross-cutting area of corrective action because although this

issue was identified by the NRC in Information Notice (IN) 87-59, "Potential RHR Pump

Loss," in 1987 and in Bulletin 88-04, "Potential Safety-Related Pump Loss," in 1988, the

licensee failed to take action to correct it until it was specifically identified as applying to

Davis Besse during the SSDI in 2002, and yet again during the CATI in 2003.

Description: On November 17, 1987, the NRC issued an information notice describing

two concerns identified by a Nuclear Safety System Supply vendor which had the

potential to impact safety operation of ECCS pumps. Specifically, IN 87-59 described

two concerns, the second of which involved the adequacy of the minimum flow

recirculation line capacity even for single pump operation. The IN noted that the vendor

specifically stated that these concerns might also be applicable to high pressure safety

injection pumps. On May 5, 1988, the NRC followed the IN with an NRC Bulletin

addressing the same concerns. Item 3 of the bulletin requested that licensees evaluate

the adequacy of the minimum flow bypass lines for safety-related centrifugal pumps with

respect to damage resulting from operation and testing in the minimum flow mode. It

stated that the evaluation should include consideration of both the effects of cumulative

operating hours in the minimum flow mode over the lifetime of the plant and during the

postulated accident scenario involving the largest time spent in the minimum

recirculation flow mode. It also requested that the evaluation include verification from the

pump suppliers that current minimum flow rates were sufficient to ensure that there will

be no pump damage from low flow operation.

Enclosure

40

During the SSDI, the NRC reviewed the HPI pump minimum flow capacity and raised

two concerns related minimum flow and no flow conditions. The NRC determined that

the adequacy of the minimum recirculation flow value of 35 gallons per minute (gpm)

was questionable and that there was a potentially unanalyzed condition during a small

break loss of coolant accident (LOCA). For certain small break LOCAs, the NRC

determined that the HPI pumps potentially could be required to operate under conditions

where the reactor coolant system (RCS) pressure would be very close to or possibly

greater than the pressure under which the HPI pumps could inject. During the

recirculation phase, after the contents of the borated water storage tank (BWST) were

injected, the return line to the BWST was procedurally required to be manually isolated

from the control room to prevent an unmonitored release of radiation. The HPI pumps

had a defined mission time of 30 days (720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br />) where the pumps were required to

remain operable. The licensee issued CRs 02-07684 (for the adequacy of the 35 gpm)

and 02-06702 (on the potentially unanalyzed lack of flow condition) to evaluate these

concerns.

The licensee resolved the issue of not having a minimum flow recirculation path during

the sump recirculation phase by implementing a modification to provide a new minimum

recirculation flow path for the HPI pumps via a connection through the decay heat

removal (DHR) injection line. This modification was designed to the same 35 gpm flow

rate as the original recirculation line because, in evaluating CR 02-07684, the licensee

concluded that the 35 gpm was adequate. During the 2003 CATI, the team again

questioned the adequacy of the 35 gpm minimum flow, especially in light of the 1988

Bulletin. Although the licensee had not reviewed the Bulletin response as part of their

evaluation of CR 02-07684, they resurrected the document in response to team

questions. The team determined that the licensees response to the Bulletin was based

on the results from three 10-minute vibration runs; these tests showed no appreciable

increase in vibration. The licensee also had contacted the pump vendor, who was

unable to confirm that the 35 gpm flow was adequate to ensure that HPI pumps would

not experience degradation as a result of hydraulic instability or impeller recirculation.

The team noted that industry experience indicated that long term pump minimum flow

value should be close to 25 percent of flow at the pumps best efficiency point. For the

HPI pumps, the flow at the best efficiency point was 600 gpm, which would indicate that

a minimum flow on the order of 150 gpm would be appropriate as compared to the 35

gpm which was in the licensee's design specification at the time of the inspection.

In response to the team again raising the issue on the adequacy of the HPI pump

minimum flow value of 35 gpm, the licensee wrote CRs 03-06526 and 03-06519. As

part of the investigation summary in CR 03-06526, the licensee provided evaluations by

three pump experts. These evaluations appeared to only justify continued operation

based on the effects of cumulative operating hours in the minimum flow mode over the

experienced lifetime of the plant. The team was unable to find any evaluation of the

ability of the HPI pumps to function on minimum flow during the licensee's stated

mission time of 30 days; this included any evaluation by the licensee that a shorter

mission time was appropriate for operating entirely on minimum flow. The team noted

that this issue was assigned a priority of "CF" which meant that the licensee did not

believe that any cause evaluation was required, just that the issue had to be resolved.

The licensee's basis for designating the CR as a "CF" was that the pump only had to

operate "occasionally" in the minimum flow configuration - which did not recognize the

Enclosure

41

pumps safety function. At the end of the on-site inspection, the licensee was still

evaluating the issue.

In December 2003, the team performed a limited review of the licensees evaluation of a

test performed on one of the HPI pumps. This test was run for 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> at a flow of 53

gpm. The basis for establishing a test duration of 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> appeared to be that the pump

shaft would experience a million cycles of operation and that, if pump failure was going

to occur, it should occur within that time period. However, the licensee did not either

extrapolate the number of cycles to the stated mission time of 30 days nor did they

provide any basis statement as to why 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> would be the maximum time that the

pump would spend on minimum flow. The basis for establishing the flow of 53 gpm was

that it was the actual flow through the installed orifice. However, the licensee did not

extrapolate the flow back to the design basis minimum or take steps to change the

design basis. While it was highly unlikely that the pump would experience flows below

the 53 gpm for the current orifice, the team noted that this test was run on only one of

four recirculation lines (including the two new ones installed during the 13th refueling

outage). The team noted that the newly installed lines had throttle valves which could

be adjusted to a flow rate anywhere in the acceptance criteria band, including a value

well below the demonstrated flow rate. The team also noted that the surveillance test

data for the 1-2 HPI pump (the one not tested) showed the recirculation flow rates on

this pump were closer to the high end of the acceptance criteria band where the

licensee was supposed to evaluate replacement of the orifice.

As a result of the teams questions, on February 8, 2004, the licensee provided an

operability determination which addressed pump operability under the design conditions.

The licensee concluded that the HPI pumps are capable of providing the necessary flow

over the mission time of 30 days with extended periods at minimum recirculation flow.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to demonstrate that the pump could successfully perform its safety

function for the stated mission time of 30 days and under the initial design minimum flow

rate of 35 gpm by either test or evaluation prior to 2004. Since there was a performance

deficiency, the team compared this performance deficiency to the minor questions

contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports." The team concluded that the issue was more than minor because the

licensee had to perform a test to demonstrate that design basis requirements could be

met and because the test results determined that the design basis requirements needed

to be changed to ensure that the HPI pumps could perform their accident required

function. This was an issue which affected the mitigating systems cornerstone. The

team reviewed this finding in accordance with IMC 0609, "Significance Determination

Process. Although the pumps had not been tested at the minimum design flow valve,

the team was unable to conclude that the safety function of the pumps had actually

been lost. This was based on a review of surveillance test results from June 2001

through December 2003. These test results showed the lowest flow rate for either pump

to be 49 gpm. Although this was slightly outside the licensee's new operability band, the

team deemed it likely that the pumps would have performed had they been called upon.

Therefore, the team answered no to all five screening questions in the Phase 1

Screening Worksheet under the Mitigating Systems column. The team concluded the

issue was of very low safety significance (Green).

Enclosure

42

The performance deficiency of not having any recirculation lines once the BWST

emptied is addressed in Section 4OA3(6)b.3.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to verify the adequacy of the design of the

minimum recirculation line flow rate of 35 gpm. Specifically, on December 23, 2003, the

licensee determined that the minimum flow rate of 35 gpm could not be verified and the

minimum value which had been verified by a suitable testing program was 53 gpm.

Because this violation was of very low safety significance and because it was entered

into the licensees CAP as CRs 03-11268, 03-11431 and 04-01050, this violation is

being treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000346/2003010-08)

.2

Increased Dose Consequences Due to Degraded Thermal Performance

Operation of Degraded Containment Air Coolers

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance. Specifically, the licensee failed to assess an

increase in the offsite dose to the public following a postulated design basis accident

due to increased containment pressure. Following discovery, the licensee entered the

issue into its corrective action process and performed the necessary analysis. The

primary cause of this violation was related to the cross-cutting area of problem

identification and resolution, because, although the issue had been previously identified,

the licensee had failed to identify that a revised dose assessment was needed until

prompted by the NRC.

Description: In 2002, the licensee identified that the CACs were significantly degraded

and required replacement. In December 2002, the licensee issued LER

05000346/2002-008-00, which discussed the degradation. During the review of

CR 03-00120 and LER 05000346/2002-008-00 and -01, the team noted that the issue of

potentially increased offsite doses due to the degraded CACs was not addressed with a

technical basis in the evaluation of CR 03-00120. In particular, the time to reach half

containment design pressure after a design basis LOCA increased from 16.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> to

58.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> because of degraded CAC performance. The specified acceptance criteria

was that the containment pressure be reduced to 50 percent of the containment design

pressure within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> as recommended by Regulatory Guide 1.4, "Assumptions

Used for Evaluating the Potential Radiological Consequences of a Loss of Coolant

Accident for Pressurized Water Reactors." The analyses performed for the degraded

CAC operability assessment did not meet this requirement. However, the licensee

concluded in CR 03-00120 that exceeding the half containment design pressure rating

within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> had no impact on dose consequences analyzed in accordance with

Regulatory Guide 1.4 assumptions, without documenting any basis for the statement.

Enclosure

43

When first questioned by the team, the licensee acknowledged that there was no formal

dose assessment to support the conclusion documented in CR 03-00120. The licensee

then performed a calculation which indicated that, although the offsite radiological doses

increased, they were still less than the Regulatory Guide 1.4 allowables when

accounting for the increase in containment pressure. The team did not review this

calculation.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to verify that increased containment pressure due to degraded CAC

performance would not result in unacceptable offsite dose consequences. Since there

was a performance deficiency, the team compared this performance deficiency to the

minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power

Reactor Inspection Reports." The team concluded that the issue was more than minor

because the licensee had to perform calculations to show that the increased time at

higher containment pressures did not result in doses being above regulatory guide

allowables. The team reviewed this finding in accordance with IMC 0609, "Significance

Determination Process.

The team reviewed the SDP questions for reactor safety, occupation radiation safety

and public radiation safety contained in MC 0612, Appendix B, Issue Screening. The

team assessed the finding through Phase 1 of the SDP. According to the Davis-Besse

Risk-informed Inspection Notebook, the CACs had both a barrier integrity and mitigating

system cornerstone function. However, the team determined that the issue was not

covered by any of the revised oversight cornerstones and was not suitable for SDP

analysis since the finding pertained to offsite dose calculations rather than CAC

performance. Therefore, this finding was reviewed by Regional Management, in

accordance with IMC 0612. The finding was determined to be of very low safety

significance (Green) because the issue regarded increased containment pressure,

related to offsite dose consequences, and although the offsite radiological doses

increased, the values were still less than the Regulatory Guide 1.4 allowables.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to implement design control measures to

verify the adequacy of design basis calculations. Specifically, the licensee failed to

demonstrate that increased containment pressure due to degraded CAC performance

did not result in unacceptable offsite dose consequences. The licensee entered this

issue into its CAP as CR 03-03980. Because this violation was of very low safety

significance and because it was entered into the licensees CAP, this violation is being

treated as an NCV consistent with Section VI.A of the NRC Enforcement Policy. (NCV

05000346/2003010-09)

Enclosure

44

.3

Containment Air Cooler Air Flow Calculation Concerns

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to correctly

identify and translate the design basis requirements into the CACs airflow analyses and

motor horsepower sizing calculations. Following discovery, the licensee entered the

issue into its corrective action program and performed a new analysis for the motor.

The primary cause of this violation was related to the cross-cutting area of problem

identification and resolution as the licensee had previously identified issues with the

motors, but had not reviewed the design calculation of record.

Description: During review of CR 03-00120, which was the licensees collective

significance review in regard to the degraded condition of the CACs, the team also

reviewed calculation 28.003. This calculation was used to size the existing CAC motor.

The team determined that the calculation was performed in 1970 and applied design

information from the Oconee Nuclear Power Plant to Davis-Besse without correction for

actual Davis-Besse conditions. The NRC team questioned the design values for system

resistance, airflow, and density used in the calculation for sizing CAC motors since there

was no reference to Davis-Besse equipment or systems.

Calculation 28.003 specified a requirement for a 45 horsepower motor, whereas at

Davis-Besse, a 40 horsepower motor was actually installed. In addition, the density

used in calculation 28.003 was different than that used for the postulated breaks

analyzed in calculation C-NSA-060.05-010. For example, C-NSA-060.05-010, the

computed density profile remained at or below 0.132 pounds per cubic foot (lb/ft3) for

the first 6 seconds, increased to 0.152 lb/ft3 from 7 to 16 seconds, then dropped to

0.132 lb/ft3 at approximately 250 seconds. In contrast, calculation 28.003 used the less

conservative density profile of 0.132 lb/ft3 throughout. Following the teams questioning,

the licensee performed a new calculation which showed that the CAC motors were

appropriately sized.

The team also noted that the vendor who supplied the CAC motors had submitted a

Part 21 notice to the licensee in May 2002. According to LER 05000346/2002-008, this

issue was entered into the CAP but was determined to not be of significance due to the

CAC motors being refurbished as part of the overall CAC refurbishment. The team

considered this to be an example of poor engineering response to an issue specifically,

the licensee had determined that the CAC motors needed to be refurbished, but had

either not looked at the design basis calculation for the motors prior to beginning the

refurbishment, or had not performed an adequate review.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to analyze CAC fan sizing with respect to actual airflow, air density,

pressure drop, and motor size. Since there was a performance deficiency, the team

compared this performance deficiency to the minor questions contained in Appendix B,

"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team

concluded that the issue was more than minor because the licensee had to revise the

associated calculation to evaluate the existing motor to ensure the CACs would be able

to perform their design function. The team assessed the finding through Phase 1 of the

SDP. According to the Davis-Besse Risk-informed Inspection Notebook, the CACs had

both a barrier integrity and mitigating system function. The team determined that this

Enclosure

45

issue affected both functions. Because the issue involved both the mitigating system

and barrier integrity cornerstones, the team entered Phase 2 of the reactor safety SDP.

The team completed the Phase 2 worksheets for the following scenarios: Transients,

Transients with Loss of the Power Conversion System, Small LOCA, Loss of Offsite

Power (LOOP), Steam Generator (SG) Tube Rupture (SGTR), Main Steam Line Break

(MSLB), Loss of Instrument Air, Loss of a 4 kilovolt (kV) Bus, Loss of DC Buses D1P

and D2P and Loss of One Emergency AC Train. Completion of these worksheets

resulted in two sequences rated as "12", three sequences rated as "11", four sequences

rated as "10", two sequences rated as "9", and three sequences rated as "8". This

information was entered into the "Counting Rule Worksheet" and a final evaluation was

obtained that the issue was of very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to this requirement, the licensee failed to correctly translate the design basis

into specifications, drawing, procedures, and instructions. Specifically, the licensee

failed to correctly identify and translate the design basis requirements such as actual

airflow, air density, pressure drop, and motor size, into the CAC airflow analyses and

motor horsepower sizing calculations that demonstrated the ability of the safety-related

CACs to deliver the required design basis air flow rate to the containment during an

accident. The licensee entered this issue into its CAP as CR 03-07009. Because this

violation was of very low safety significance and because it was entered into the

licensees CAP, this violation is being treated as an NCV consistent with Section VI.A of

the NRC Enforcement Policy. (NCV 05000346/2003010-10)

.4

Accumulator Sizing Calculation Errors

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to

implement effective design control measures to check and verify the adequacy of the

design basis calculation performed for sizing the new accumulators used to hold the SW

containment isolation valves closed on a loss of instrument air. Following discovery, the

licensee entered the issue into its corrective action program, revised the calculations,

and changed the accumulator medium from compressed air to nitrogen.

Description: In 2002, SSDI team identified a NCV for failing to correctly translate the

design basis requirements for sizing of the safety-related backup air supplies for

containment isolation valves SW-1356, SW-1357, and SW-1358 into the design. The

licensees corrective action was to install new accumulators sized to hold the valves

closed. The team reviewed several revisions of calculation C-ME-011.06-007 which

sized the new accumulators.

Enclosure

46

The team identified numerous errors in the calculation which required the calculation to

be revised. For example, in Revisions 0 and 1 of the calculation, the new accumulators

were intended to be filled with air as the licensee thought the valves only had to remain

closed for 30 minutes. The licensee initially did not appear to recognize that the valves

had a containment isolation design function which required the valves to remain closed

for 30 days until questioned by the team during the inspection. Following the teams

questions, the licensee changed the design to require that the new accumulators be

filled with nitrogen rather than air. In the last revision reviewed, the calculation

erroneously used the ideal gas law equations when sizing the nitrogen bottles without

consideration of the compressibility of nitrogen at a pressure of 2000 pounds per square

inch (psig). The calculation also indicated that the valve actuators were double acting

when other documents indicated that actuators were single acting. Additionally, the

calculation could not stand alone without recourse to the author because certain

calculation steps were missing. The licensee revised the calculation to correct the

errors identified by the team. The team noted that the licensee was addressing past

operability of the accumulators separately as part of LER 05000346/2003-001. This

LER will be addressed in a separate IR.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to verify the adequacy of the design basis calculation performed for

sizing the accumulators prior to approving the calculation. Since there was a

performance deficiency, the team compared this performance deficiency to the minor

questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor

Inspection Reports." The team concluded that the issue was more than minor because

the licensee had to re-perform calculations and had to change the modification design

from having accumulators containing pressurized air to accumulators containing

pressurized nitrogen. The team reviewed this finding in accordance with IMC 0609,

"Significance Determination Process.

The team reviewed the SDP questions for reactor safety, occupation radiation safety

and public radiation safety contained in MC 0612, Appendix B, Issue Screening. The

team assessed the finding through Phase 1 of the SDP. However, the team determined

that the issue was not covered by any of the revised oversight cornerstones and was,

therefore, not suitable for SDP analysis. This determination was based on the issue

affecting containment isolation valves which provide a barrier to breach of containment

and potential offsite dose consequences. Therefore, this finding was reviewed by

Regional Management, in accordance with IMC 0612. The finding was determined to be

of very low safety significance (Green) because the issue regarded increased

containment pressure and related to offsite dose consequences.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Enclosure

47

Contrary to the above, the licensee failed to implement design control measures to

check and verify the adequacy of the design basis calculation performed for sizing the

accumulators used to hold containment isolation valves closed on a loss of instrument

air. The licensee entered the issue into its CAP as CR 03-06556. Because this violation

was of very low safety significance and because it was entered into the licensees CAP,

this violation is being treated as an NCV consistent with Section VI.A.1 of the NRC

Enforcement Policy. (NCV 05000346/2003010-11)

.5

Inadequate Blowdown Provisions for Containment Isolation Valve Accumulators

Introduction: The team identified a performance deficiency involving the licensee's

failure to initiate a CR or to implement corrective actions to address a previously

identified NRC finding. Following discovery, the licensee entered the issue into its

corrective action program.

Description: Non-Cited Violation 05000346/2002014-01b was issued by the NRC during

the 2002 SSDI to document that there were no provisions to blow down the SW

containment isolation valve accumulators although USAR Section 9.3.1.5 stated that the

accumulators contained a provision to allow removal of excessive moisture. IR

54-346/2002014 documented that this NCV was captured in the licensee's CAP as

CR 02-07750. When the CATI team reviewed CR 02-07750, the team determined that

the CR did not document this concern. The licensee was unable to identify any CR

which addressed the NCV and could not find any indication that corrective actions had

been taken to address the issue.

The valves discussed in the NCV were containment isolation valves equipped with

backup air accumulators (air volume tanks). These valves had dual safety functions in

that they were required to open during a LOCA to provide maximum SW flow through

the CACs as well as being required to close to provide containment isolation. The team

noted that, although the licensee was in the process of designing the new accumulators,

they had not specifically considered or addressed providing accumulator blowdown

capability. The failure to include blowdown provisions meant that any moisture intrusion

into the accumulator would not be identifiable and would not be removable. This would

result in the reduction in the amount of air available to maintain the containment

isolation valves closed and would result in rust and other debris in the accumulator.

In response to the teams finding, the licensee issued CR 03-02475 on March 28, 2003,

to document this concern and ensure that it was included in the Davis-Besse CAP. The

licensee informed the team that MOD 99-0039, Revision 1 should address this concern,

when completed. In November 2003, the team reviewed the corrective actions

generated for CR 03-02475 and determined that the specified modification had been

canceled and a new modification package generated. Based on the wording in the

corrective action cancellation, it was not apparent that the blowdown issue was

reassessed as part of the new modification.

The team independently determined that, due to the change in accumulator medium

from air to nitrogen, that there was no longer any need for blowdown provisions. While

the NRC concluded that the lack of blowdown no longer presented a safety issue.

Enclosure

48

Analysis: The team determined that a performance deficiency existed because the

licensees program required it to initiate a CR and implement corrective actions to

address NRC identified NCVs. Since there was a performance deficiency, the team

compared this performance deficiency to the minor questions contained in Appendix B,

"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team

concluded that the issue was minor because the licensee changed the accumulator

medium to one which would not contain moisture, such that the failure to take corrective

actions had no consequences.

Enforcement: The failure to take corrective actions for an identified condition adverse to

quality constituted a violation of 10 CFR Appendix B, Criterion XVI, which has minor

significance and is not subject to enforcement action in accordance with Section IV of

the NRCs Enforcement Policy.

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case due to the issue not initially

being in the CAP and then due to the corrective actions being canceled without

reconciliation of the original issue. Additionally, the underlying cause is similar to that of

other findings in this report.

.6

Non-conservative Calculation Used in Design Analysis to Determine Required

Service Water Makeup Flow to Component Cooling Water

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance. Specifically, the licensee failed to consider worst

case minimum pressure differential between SW and component cooling water (CCW)

systems when determining required SW makeup flow to the CCW system heat

exchangers. Following discovery, the licensee entered the issue into its corrective

action process and performed the necessary calculations. The primary cause of this

violation was related to the cross-cutting area of human performance because the

licensee used test data collected during normal operation rather than taking the worst

case design conditions and because there was a lack of rigor in the calculation review

process.

Description: Hydraulic calculation C-ME-011.01-140 was developed as part of a

corrective action to CR 02-07378. This calculation determined the pressure differential

required in the SW line for makeup to the CCW system to create a minimum flow of

30 gpm. This flowrate was used to estimate the stay time and exposure rate while using

SW to makeup to the CCW system. The NRC team reviewed the calculation, and

determined that it was non-conservative in that it did not consider worst-case minimum

pressure differential between SW and CCW systems during accident conditions, but

used test data collected during normal operation. In addition, the calculation assumed a

fully turbulent fouling factor for clean piping. Finally, there was a minor math error in the

calculation. Although the math error did not appreciably affect the results of the

calculation, it indicated a lack of rigor in the calculation review process. In response to

the NRC's questions, the licensee performed additional calculations. The licensee

stated that these new calculations showed that, even with the lower predicted differential

pressures while in the accident alignment, the makeup capability of SW to CCW

Enclosure

49

exceeded the acceptance criteria. The team did not review these additional

calculations.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to verify the adequacy of the design basis calculation performed for the

SW and CCW system interface. Since there was a performance deficiency, the team

compared this performance deficiency to the minor questions contained in Appendix B,

"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team

concluded that the issue was more than minor because the licensee had to perform a

new calculation to demonstrate that the SW flow to CCW was adequate to perform its

design function. This finding was considered a design deficiency which affected the

mitigating systems cornerstone. The licensee determined that the SW flow was

adequate to perform its design function and was operable The team reviewed this

finding in accordance with IMC 0609, "Significance Determination Process, and

answered no to all five screening questions in the Phase 1 Screening Worksheet

under the Mitigating Systems column. The team concluded the issue was of very low

safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to implement design control measures to

check and verify the adequacy of the design basis calculation performed for the

SW/CCW system crosstie hydraulic analyses for all postulated accidents. The licensee

entered the issue into its CAP as CR 03-04010. Because this violation was of very low

safety significance and because it was entered into the licensees CAP, the violation is

being treated as a NCV, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000346/2003010-12)

.7

Calculation Concerns for Service Water Pump Room Ventilation System

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to verify the

adequacy of the design of the SW pump room ventilation system. Following discovery

that the design basis calculations were non-conservative, the licensee entered the issue

into its corrective action program, re-performed the calculations, and made appropriate

modifications to correct the issues. The primary cause of this violation was related to

the cross-cutting area of problem identification and resolution because the licensee

failed to correct all of the originally identified issues until identified by team.

Description: During the SSDI inspection in 2002, the NRC identified a concern

regarding calculation 67.005. The calculation analyzed the heat loads in the SW pump

room and the ability of the ventilation system to maintain the pump room temperatures

within a required operating range. The team determined that the calculation contained

Enclosure

50

multiple non-conservative attributes, including failing to analyze heat loss through open

penthouse louvers during the winter, and failing to account for heat load contribution of

diesel driven fire pump during the summer. The licensee initiated CR 02-07188 to

document this issue.

The calculation was revised to address these concerns and was issued as Revision 4 in

early 2003. At the same time, another CR, 02-08281, was issued because

CR 02-07188 failed to do an extent of condition review to verify the adequacy of the SW

ventilation system for all operating conditions. The extent of condition review was

reported to have included a walkdown of the SW pump room and review of the revised

SW ventilation calculation.

Upon review of the revised calculation in 2003, the team noted that the summer

maximum analyzed temperature in the pump house did not include the heat load

contribution of the diesel driven fire pump, which was one of the deficiencies noted in

the earlier revision to the calculation. This deficiency was not addressed in the new

revision to the calculation, either by including it or by providing a rationale for excluding

the heat load. The team noted that the licensee had previously had to take actions to

open the diesel generator room doors and provide alternate ventilation during the

summer months. The new calculation also concluded that the penthouse louvers had to

be modified (blocked) for winter operation. The NRC team noted that past operability

had been assured for winter operation by regularly recording pump room ambient

temperature.

Calculation C-NSA-085.00-002, Auxiliary Steam Blowdown in the Intake Structure,

concluded that the maximum temperature within the SW pump room was 109

degrees F. This temperature was not considered a significant difference from the

normal operating temperature in the room. Additionally, the safety related equipment in

the room was specified for operation in an environment with 100 percent relative

humidity, which would be experienced in the room during a postulated steam break. An

evaluation performed in CR 02-05262 concluded that the amount of condensing

moisture would fill the smallest electrical junction box by only 0.05 inches. Therefore,

the functionality of the cables and connections was not likely to be affected. The team

also noted that the licensee had initiated engineering change request (ECR) 02-0682 to

remove the auxiliary steam line from the SW pump room, although it stated that this

modification was an enhancement which was not required.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to verify the adequacy of the SW pump room ventilation system for all

operating conditions. Since there was a performance deficiency, the team compared this

performance deficiency to the minor questions contained in Appendix B, "Issue

Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded that

the issue was more than minor because inadequacies in the calculations identified during

the 2002 SSDI resulted in a modification to ensure winter operation was within the

allowable temperature range, and because the revised calculation did not include all the

summer heat loads which could potentially impair the SW pump room ventilation system.

This was a design issue which affected the mitigating systems cornerstone. The team

reviewed this finding in accordance with IMC 0609, "Significance Determination Process,

and answered no to all five screening questions in the Phase 1 Screening Worksheet

Enclosure

51

under the Mitigating Systems column. The team concluded the issue was of very low

safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to implement design control measures to

check and verify the adequacy of the design. Specifically, the licensee failed to verify

the adequacy of the SW pump room ventilation system for all operating conditions.

The licensee entered this issue into its CAP as CRs 02-07188 and 03-06870. Because

this violation was of very low safety significance and because it was entered into the

licensees CAP, this violation is being treated as a NCV consistent with Section VI.A.1 of

the NRC Enforcement Policy. (NCV 05000346/2003010-13)

.8

Inadequate Service Water System Flow Analysis

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance. Specifically, the licensee failed to ensure that the

SW system could perform its design function under all required conditions. Following

discovery, the licensee entered the issue into its corrective action program and

performed the necessary calculations.

Description: In IR 05000346/2002014, several URIs were identified dealing with the SW

system and ultimate heat sinks. These deficiencies included failure to account for the

lowest acceptable performance of the SW pumps, failure to consider the USAR

described single failure of the forebay return valve to open, failure to include the design

basis strainer resistance, and strainer blowdown losses. Additionally, the design basis

lowest ultimate heat sink level was not used and the flow diverted to the AFW was not

considered. Because of these deficiencies, the ability of the system to provide the

required design basis flows to the safety-related heat exchangers could not be verified.

In response to the issues identified by the SSDI, as well as other issues identified

internally, the licensee determined that there was not sufficient design basis

documentation to demonstrate operability of the SW system under all required

conditions. The licensee had a consultant perform two new calculations,02-113 and

02-123, to address a large number of SW flow issues, including those issues discussed

above.

The team reviewed these calculations and noted that the calculations determined that,

under a certain combination of design basis conditions, design basis flow rates and

pump net positive suction head (NPSH) were not achievable. The specific combination

included having design basis low ultimate heat sink levels, design basis high SW

temperatures and the SW strainers going into backwash while the system was

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responding to a design basis accident. The team determined that the strainer operation

was automatic such that this set of circumstances was one which the licensee should

have included as part of its design basis.

The team noted that the licensee had reviewed and approved the calculation without

comment. This issue negatively reflected on the adequacy of the licensees engineering

department to oversee the engineering contractor performing the calculations and on

the engineering staffs ability to identify engineering issues and non-conforming

conditions. The team independently evaluated the issue and determined that the

system would most likely be able to perform its design function as the inadequate

conditions would only exist for short periods of time. The licencee initiated CR 03-03977

to revise the calculations. Following evaluation of CR 03-03977, the licensee concluded

that the SW system was able to perform its safety related function. The team agreed

with the licensees conclusions.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to ensure the adequacy of the SW system to supply required flow rate to

safety related components and failed to ensure the required NPSH for the SW pumps.

Since there was a performance deficiency, the team compared this performance

deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC

0612, "Power Reactor Inspection Reports." The team concluded that the issue was

more than minor because the licensee did not initially have a calculation which

demonstrated that the SW system could fulfill its design function under design basis

conditions and when a calculation was subsequently prepared, system deficiencies were

not evaluated to ensure that the safety function could be met. This was a design issue

which affected the mitigating systems cornerstone. The licensee concluded that the SW

system had been able to perform its safety function. The team reviewed this finding in

accordance with IMC 0609, "Significance Determination Process, and answered no to

all five screening questions in the Phase 1 Screening Worksheet under the Mitigating

Systems column. The team concluded the issue was of very low safety significance

(Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to ensure that design requirements were

correctly translated into specifications, drawings, procedures, and instructions.

Specifically, the licensee did not have design calculations to show the SW system could

perform its required safety function under design basis conditions.

The licensee entered the issue into its CAP as CRs 02-06337, 03-07006, and 03-07042.

Because this violation was of very low safety significance and because it was entered

into the licensee CAP, this violation is being treated as a NCV, consistent with

Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000346/2003010-14)

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.9

Inadequate Flooding Protection for the Service Water System

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to have

provisions in place to protect the SW pump room from flooding. Following discovery,

the licensee placed the issue in its corrective action program, evaluated it and put

procedures in place to address the issue.

Description: During the SSDI in 2002, the NRC identified that no procedures were in

place to isolate equipment open for maintenance in the SW pump room that could flood

the room in the event of high lake water level. USAR Section 2.4.8.2 stated, "The

Probable Maximum Flood Water is elevation 583.7 feet..." USAR Section 9.2.1.3

stated, "In the event of high water levels,...the pump room is sealed to prevent flooding."

Finally USAR Section 3D.1.4, "[General Design Criteria (GDC)] Criterion IV -

Environmental and Missile Design Basis," stated, "These [safety-related] structures,

systems, and components are appropriately protected against dynamic effects...and

discharging fluids, that may result from equipment failures and from events and

conditions outside the nuclear power unit." Therefore, the NRC questioned whether the

SW system was adequately protected against flooding effects that could result from

high lake water levels, from internal flooding, and from other threats to the system that

could result from failure of non-seismically qualified equipment, as described in the

USAR.

In response to this concern, the licensee determined that operator actions were

necessary in order to ensure that the USAR statements were met. In order to ensure

that the operator actions occurred, several changes to operating procedures were

required. These procedural actions were taken. During the 2003 CATI, the team

verified that the corrective actions were implemented and appropriately resolved.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to translate design basis requirements into procedures for flood

protection in the SW pump room. Since there was a performance deficiency, the team

compared this performance deficiency to the minor questions contained in Appendix B,

"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team

concluded that the issue was more than minor because the licensee had to make

procedural changes in order to ensure that safety-related equipment was capable of

performing its safety functions. This was a procedural deficiency which affected the

mitigating systems cornerstone. The licensee determined that the system remained

operable since the deficiency only dealt with a lack of procedural guidance. The team

reviewed this finding in accordance with IMC 0609, "Significance Determination

Process, and answered no to all five screening questions in the Phase 1 Screening

Worksheet under the Mitigating Systems column. The team concluded the issue was of

very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

Enclosure

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use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to correctly translate the design basis into

procedures. Specifically, the licensee failed to have procedures in place to isolate

equipment opened during maintenance in the SW pump room that could potentially

flood the room in the event of rising lake water level.

The licensee had previously entered this issue into its CAP as CR 02-07714. Because

this violation was of very low safety significance and because it was entered into the

licensees CAP, the violation is being treated as a NCV, consistent with Section VI.A of

the NRC Enforcement Policy. (NCV 05000346/2003010-15)

.10 Inadequate Service Water System Flow Balance Testing Procedure

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,

having very low safety significance (Green). Specifically, the licensee failed to account

for a number of conditions in the SW system flow balance testing procedures. Following

discovery, the licensee placed the issue in its corrective action program, evaluated it and

put procedures in place to address the issue.

Description: Surveillance procedures DB-SP-03000 and 03001, "Service Water

Integrated Train I (II) Flow Balance Procedure," were performed every refueling outage

to balance the system flows. During the 2002 SSDI, the NRC identified that this

procedure did not establish flows to the safety-related heat exchangers based on

worst-case design basis conditions, such as degraded SW pumps, lowest ultimate heat

sink (UHS) level, highest resistance SW system lineup, or system resistance

degradation. Further, no analyses existed that established the test acceptance criteria

for design basis conditions. Therefore, the flow balance procedure did not verify that

the system was capable of providing the required flows to its safety-related heat

exchangers under design basis conditions.

The licensee performed SW flow model calculations that conservatively predicted the

required flow to each safety-related load. The model addressed all SW branch lines in

service during various accident scenarios and accounted for the flow rate issues

described in CR 02-06337. Separately, the licensee computed the required instrument

inaccuracies for the instrumentation used during the SW flow balance.

However, the licensee's design organization did not ensure that this information was

properly transmitted to the plant engineering group in a format that would ensure that

the procedures had adequate acceptance criteria. The design engineering organization

did not perform a formal calculation which documented the minimum acceptance criteria

to ensure that the test procedure would demonstrate that the SW flows met their design

basis requirements. Instead, design engineering transmitted the design information in

two separate evaluations which then had to be combined by plant engineering and

corrected for the instrument measurement uncertainty. Because the plant engineering

department had to interpret the results from design engineering, the plant engineering

personnel applied considerable conservatism when establishing the test acceptance

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criteria. The licensee issued CR 03-07006 to provide a design record file for test

acceptance criteria.

During SW testing performed in the summer and fall 2003, the licensee determined that

the newly established test acceptance criteria could not be met for some components.

This resulted in numerous CRs being written and the design engineering organization

having to prepare a number of operability evaluations justifying the use of lower

acceptance criteria. The team determined that the design engineering failure to

establish appropriate acceptance criteria prior to the SW testing occurring contributed to

the number of CRs and subsequent operability evaluations.

The team determined that the licensee planned to perform a flow balance twice each

refueling outage, once on as found basis, and once on an as-left basis. Collecting

as-found data would provide evidence that the SW system branch flows were adequate

during the previous operating cycle to remove the design basis heat loads. The team

considered this a positive step by plant engineering to ensure operability of the SW

system.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to properly account for a number of required conditions in the SW system

flow balance testing procedure. Since there was a performance deficiency, the team

compared this performance deficiency to the minor questions contained in Appendix B,

"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team

concluded that the issue was more than minor because procedural changes were

necessary in order to ensure that the safety-related SW system branch flow rates were

adequate for the system to perform its safety functions. The team assessed the finding

through Phase 1 of the SDP. This was a design issue which affected the mitigating

systems cornerstone. At the end of the inspection, the licensee was performing a new

flow balance. The licensee concluded that the system was previously capable of

meeting its design requirements. The flow balance test results were reviewed by the

resident inspectors and document in IR 2003025. The team reviewed this finding in

accordance with IMC 0609, "Significance Determination Process, and answered no to

all five screening questions in the Phase 1 Screening Worksheet under the Mitigating

Systems column. The team concluded the issue was of very low safety significance

(Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI, "Test Control, requires, in

part, that a test program shall be established to assure that all testing required to

demonstrate that structures, systems, and components will perform satisfactorily in

service is identified and performed in accordance with the written test procedures which

incorporate the requirements and acceptance limits contained in the applicable design

documents.

Contrary to the above, the licensee failed to adequately test the SW system because

the licensees SW system flow balance testing procedure failed to account for a number

of required conditions. The testing failed to verify that adequate flow was provided to

safety related components under all accident conditions.

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The licensee entered the issue into its CAP as CRs 02-06064 and 03-07006. Because

this violation was of very low safety significance and because it was entered into the

licensees CAP, this violation is being treated as a NCV consistent with Section VI.A of

the NRC Enforcement Policy. (NCV 05000346/2003010-16)

.11 Service Water Discharge Path Swapover Setpoint

Introduction: The team identified a violation of 10 CFR Part 50, Appendix B, Criterion III,

involving the licensee's failure to provide a basis for the setpoint to swap the service

water system discharge path. This issue was previously identified as an NCV in IR

05000346/2002014 and the corrective actions taken by the licensee failed to correct the

originally identified condition. The primary cause of this violation was related to the

cross-cutting areas of problem identification and resolution and human performance,

because the licensee did not recognize that the corrective actions taken needed to

restore compliance with the identified violation of NRC requirements.

Description: The 2002 SSDI identified a Green finding and NCV of 10 CFR Part 50,

Appendix B, Criterion III, regarding the licensee's failure to provide a calculational basis

for the 50 psig setpoint to swap SW system discharge path. The licensee did not

contest the violation and entered the issue into the corrective action system as

CR 02-07802. During the CATI, the team reviewed the evaluation and corrective

actions taken for this NCV. The team determined that the licensee had evaluated the

condition and confirmed that no analysis initially existed. The evaluation reviewed by

the team was initially approved on March 9, 2003 and had a corrective action also

accepted on March 9, 2003. This evaluation focused on the fact that no setpoint

calculation existed which showed that instrument uncertainty values had been properly

incorporated, not on providing the calculational basis for the 50 psig setpoint itself. The

team determined that this evaluation and proposed corrective action were not

responsive to the violation identified during the SSDI.

On November 10, 2003, the licensee provided the team a revised copy of CR 02-07802.

The originally approved condition report was apparently rejected and replaced with a

new evaluation and new corrective actions on March 30, 2003. The new evaluation

documented a vendor calculation which showed that with the 50 psig setpoint, there

would be inadequate flow to certain safety related components under design basis

conditions. The new evaluation also concluded that the setpoint was adequate if a

failure of the non-seismically qualified discharge piping did not have to be postulated

during a loss of coolant event. Relying upon this latter conclusion, the licensee

determined that the 50 psig setpoint was acceptable. The team did not agree with the

licensees reliance on non-seismically qualified piping to ensure that safety related

components had adequate flow. Therefore, the team determined that the revised

evaluation still did not address the SSDI violation in that the calculational basis for the

50 psig issue still did not exist.

The team noted that the evaluation contained in the revised CR 02-07802 was similar to

that documented in CR 02-05748. Both CRs articulated a view that, unless there was a

seismic event, non-seismic lines did not have to be assumed to have failed. The team

questioned this premise, based on the information in 10 CFR Part 50, Appendix A,

GDC. The team noted that the licensee had committed to following the draft version of

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these criteria, as documented in NUREG 0153, and committed to in the USAR. Draft

General design criteria 2, in that NUREG, stated, in part, that components important to

safety were to be designed to withstand the effects of natural phenomena without loss

of their safety function.

The team presented this information to the licensee engineers as part of the review of

CR 02-05748. The engineers sought the advice of the regulatory assurance department

via CR 03-04018. The regulatory assurance department responded, in part, that, "It

was not appropriate to apply the single failure criterion to non-safety systems,"

confirming the team position. The licensee then wrote a new CR (03-06507) and took

compensatory measures to close the SW discharge valve leading to the cooling tower.

The licensee also stated in CR 03-06507 that the issue involved application of single

failure assumptions for existing systems. The team noted that this appeared to be a

continuation of the misunderstanding of application of design basis assumptions.

Following the inspection, the licensee performed a PRA study on the likelihood of failure

of the non-safety-related piping and then applied the results of this analysis to justify the

issue described in CR 02-07802. As this analysis was performed significantly after the

end of the inspection, it was not reviewed by the team, and the team was not able to

evaluate the impact of this analysis on the licensing basis of the plant.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to correct a previously identified violation of NRC requirements. Since

there was a performance deficiency, the team compared this performance deficiency to

the minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power

Reactor Inspection Reports." The team concluded that the issue was more than minor

because the licensee had not corrected a previous violation and was relying on

non-safety-related equipment to perform a safety function under design bases

conditions.

The previously identified violation was evaluated in IR 05000346/2002014 as having

very low safety significance (Green). This assessment has not changed. This finding

was reviewed by Regional Management, in accordance with IMC 0612. The finding was

determined to be of very low safety significance and concluded that the violation could

be categorized as Green.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, as of August 12, 2003, the licensee failed to verify that the

design of the SW system discharge path swapover setpoints were adequate.

Specifically, the analysis performed by the licensee showed that the established

setpoints were not adequate and the evaluation of the analysis accepted the inadequate

setpoint based on non-safety-related equipment performing a safety-related function

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under design basis conditions. Neither the analysis nor the evaluation corrected the

non-conforming condition previously identified in IR 05000346/2002014.

This is a violation of 10 CFR Part 50, Appendix B, Criterion III. The NRC Enforcement

Policy,Section VI.A.1, provides guidance on dispositioning of violations. Normally,

violations of very low safety significance are not cited. However, the Enforcement Policy

notes four conditions under which an issued notice of violation with a reply will be

considered. The first of these conditions is, "The licensee failed to restore compliance

within a reasonable time after a violation was identified." As the corrective action

generated in response to the NCV did not restore compliance, this condition has been

met. (VIO 05000346/2003010-01)

.12 Service Water Discharge Check Valve Test Acceptance Criteria

Introduction: The team identified a violation of TS 4.05a an 10 CFR 50.55a, having very

low safety significance. Specifically, the licensee failed to ensure that the service water

discharge check valve was tested in accordance with ASME Code. The primary cause

of this violation was related to the cross-cutting areas of problem identification and

resolution and human performance, because the licensee did not recognize that the

corrective actions taken needed to ensure compliance with NRC requirements.

Description: The 2002 SSDI described a Green finding and NCV of 10 CFR Part 50,

Appendix B, Criterion XVI, regarding the licensees failure to adequately correct the SW

pump discharge check valve acceptance criteria. This was entered into the licensees

corrective action system as CR 02-07657. The team determined that the licensee

evaluated the concern in the NCV and determined that the valves were full open at flow

rates greater than 7270 gpm. Therefore, the licensee concluded that no corrective

actions to the procedure were necessary. The CR evaluation stated that CR 02-05784

would address the differences in the stated flow rates in the USAR and system

description. No formal calculation was prepared to support the 7270 gpm value and no

corrective actions were generated for the CR. This CR was accepted as being ready for

closure on January 28, 2003.

The team noted the licensees evaluation of the flow rate at which the valves were full

open could not be reproduced as it relied on oral information provided by the valve

vendor. The team identified that numerous check valve failures had been identified in

the industry which were not detected during inservice testing of check valves to values

less than the required accident flow rate. Furthermore, the evaluation did not follow any

of the methods listed in GL 89-04, "Guidance on Developing Acceptable Inservice

Testing Programs" or NUREG 1482, "Guidelines for Inservice Testing Programs at

Nuclear Power Plants" for ensuring that the valves were full open.

The team reviewed the licensees technical specification 4.05a and confirmed that the

licensee was required to test their check valves in accordance with the ASME Code for

Operation and Maintenance of Nuclear Power Plants (ASME OM Code) as required by

10 CFR 50.55a. The team confirmed that the licensee was committed to the 1996

Addenda of the OM Code. Section ISTC 4.5.4a of this addenda stated that check

valves which had a safety function to open were to be tested by initiating flow and

observing that the valve had traveled to the full open position or to the position required

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to perform its intended function. Using the guidance in GL 89-04, the team ascertained

that "the position required to perform its intended function" would be one which passed

the required accident flow rate.

The team noted that the GL provided guidance for cases where a full flow test on a

check valve could not be performed. For these cases, the licensee should submit a

relief request from the ASME requirements to the NRC and have the request granted

prior to implementing the requested relief.

Based on the above, the team concluded that the licensees evaluation in CR 02-07657

was inadequate in it did not demonstrate that 7270 gpm flow would ensure that the

check valve was in the full open position. Because of this inadequate evaluation, the

licensee did not take appropriate corrective actions to bring the surveillance procedure

acceptance criteria into compliance with the requirements.

The team further reviewed CR 02-05784 and noted that it did not contain any references

to CR 02-07657 and did not address the corrective actions which CR 02-05784 had

stated would be addressed by the CR. Specifically, there were no corrective actions

addressing the USAR and system description issues as stated by CR 02-07657.

Furthermore, the implementing organization had determined that the initially

recommended corrective actions to 02-05784 were not necessary and had

recommended that they be canceled, although this recommendation had not been

formally accepted by the end of the inspection. The team ascertained that the accident

analyses of record required a SW flow rate of approximately 10,300 gpm in order to

ensure sufficient cooling of safety related systems.

Following the on-site inspection, the team performed a limited review of CR 03-07656.

This CR noted that the SW pump #3 discharge check valve had not met the

procedurally required acceptance criteria. The operability evaluation for this CR

accepted the deficiency as operable based on the inadequate evaluation in CR 02-

07657. Use of the evaluation from CR 02-07657 to justify operability resulted in the

licensee using an alternate means of verifying that the check valve was full open without

obtaining the necessary NRC approval for relief from the Code requirements.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to demonstrate that the check valve could perform its intended function in

accordance with NRC requirements. The team concluded that the issue was more than

minor because the inadequate test acceptance criteria allowed the licensee to accept a

check valve as performing its intended function at less than full system flow. The

licensee did not request NRC approval to use an alternate means of demonstrating the

valve was capable of performing its intended function. The team concluded that the

issue involved traditional enforcement because the licensee had not sought NRC

approval prior to using an alternate means of demonstrating that a check valve could

perform its intended function.

In 2002, the issue was determined to be of very low safety significance. However,

because the licensee accepted a valve as being full open with less than the accident

required flow rate, the team re-evaluated the safety significance. The team determined

that the licensee had an operability determination which concluded that the SW system

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was operable but degraded, as it could not achieve design flow rates. This operability

determination was reviewed by the resident inspectors and determined to be

acceptable, as documented in IR 05000346/2003025. The team concluded that, as the

valve was part of the SW system, it was covered by this operability determination. As

the licensee concluded the system was operable, the issue screened out of the Phase 1

worksheet (Green).

Enforcement: Technical specification 4.05a requires, in part, that the licensee perform

inservice testing of valves in accordance with the ASME OM Code and applicable

addenda as required by 10 CFR 50, Section 50.55a.

Title 10 CFR 50.55a(f)(4) requires, in part, that, during successive 120 month intervals,

a licensee must comply with the requirements in the latest edition and addenda listed in

paragraph (b) of 10 CFR 50.55a 12 months prior to the start of the 120 month interval.

Paragraph 50.55a(f)(5)(i) requires that the inservice test program be revised as

necessary to meet the requirement of paragraph 50.55a(f)(4). Paragraph

50.55a(f)(5)(iii) requires that if a licensee determines that conformance with certain code

requirements is impractical, the licensee is to submit information to support the

determination, in accordance with 10 CFR 50.4.

The ASME OM Code, 1996 addenda, Section ISTC 4.5.4(a) requires, in part, that check

valves be exercised by initiating flow and observing that the obturator traveled to its full

open position. The NRC approved use of the 1995 Code edition through the 1996

addenda for the third inservice testing 120-month interval on March 28, 2003 . Prior to

that date, the licensee was committed to the 1986 Edition (no Addenda) of the ASME

Boiler and Pressure Vessel Code,Section XI. The 1986 Code Edition contains similar

requirements.

Contrary to the above, on September 12, 2003, and other dates, the licensee did not

observe by a direct indicator or other positive means that the ASME Class 3 service

water pump discharge check valve obturator traveled to its full open position during its

quarterly surveillance test. Specifically, on September 12, 2003, the licensee observed

a flow rate of 9718 gpm through valve SW-19, which was less than the test acceptance

criterion of 10,000 gpm, and less than the approximately 10,300 gpm used in the

licensees most recent accident analysis. Observing flow rates less than required for the

valve to perform its safety function was not a positive means to determine that the

obturator traveled to its full open position and no other direct indicator or positive means

was used.

This is a violation of TS 4.05a and 10 CFR 50.55a. The NRC Enforcement Policy,

Section VI.A.1, provides guidance on dispositioning of violations. Normally, violations of

very low safety significance are not cited. However, the Enforcement Policy notes four

conditions under which an issued notice of violation with a reply will be considered. One

of these conditions is, "The licensee failed to restore compliance within a reasonable

time after a violation was identified." As the CR addressing this issue was accepted for

closure without restoring compliance by either revising the test acceptance criteria or

submitting a license amendment to the NRC to use an alternate means of verifying that

the valves were full open, this condition has been met. At the time of the exit, no new

CR had been written to address this issue. (VIO 05000346/2003010-02)

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.13 Lack of Design Basis Calculations to Support Service Water Single Failure

Assumptions

Introduction: The team identified an NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance. Specifically, the licensee failed to provide an

analysis which addressed the service water valve single failure assumptions mentioned

in the updated safety analysis report. Following discovery, the licensee entered the

issue in its corrective action program. The primary cause of this violation was related to

the cross-cutting area of problem identification and resolution because the licensee had

not recognized the impact of the issue on the design basis and had not corrected it after

it was identified in 2002.

Description: In IR 05000346/2002014, two URIs were identified dealing with the

ultimate heat sinks temperature and level analyses. A concern expressed in both URIs

dealt with single failure assumptions of the SW discharge path valves to redirect flow in

the most conservative manner. These single failure assumptions were described in the

USAR as being the most limiting events for the SW system. For example, for the

maximum ultimate heat sink temperature case, a single failure of the forebay return

valve (SW 2930) to open would result in the SW discharge being directed approximately

17 feet from the intake, rather than some 500 feet away. This would increase the SW

temperature returning to the plant. For the minimum level case, a single failure of the

cooling water makeup valve (SW 2931) to close would result in water being diverted to

the cooling towers instead of being returned to the ultimate heat sink, which would lower

the available level.

Both valves were butterfly valves, and the licensee determined that the only credible

failure was an electrical failure of the valve to change position. The licensee did have

procedures which addressed the operators opening (or closing) the valves manually as

needed. The team noted that the USAR stated that the operators needed to close the

valves within three hours. However, the calculations for the ultimate heat sink maximum

temperature and minimum water level started with the valves already opened (or

closed). Because these calculations did not account for the three hour time delay, and

because the licensee did not have any calculation to support a different time period, the

team considered them to be non-conservative in regard to both maximum temperature

and minimum level. As an interim measure the licensee implemented changes to

operations procedures to control the position of the valves to address the issue. The

licensee is also performing additional review and evaluations of the facilitys

conformance with design and licensing basis documents. The actions resolved any

immediate operability concerns regarding postulated single failures with maximum

system temperatures and minimum heat sink level conditions.

The ultimate heat sink calculations supported a change to the TSs (amendment 242). The

team identified other problems with this submittal, as discussed in Section 4OA3(3)b.21.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to analyze the effects on the ultimate heat sink of the forebay return valve

not opening or of the cooling water makeup valve not closing for the time period

necessary for an operator to take action. Since there was a performance deficiency, the

team compared this performance deficiency to the minor questions contained in

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Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The

team concluded that the issue was more than minor because the current calculations

were non-conservative and the licensee was not able to demonstrate that the SW

system could perform its safety function under design basis conditions. This was a

design issue which affected the mitigating systems cornerstone. The team determined

that it was unlikely that the SW system would not function during a design basis

accident, as there would need to be the unlikely combination of both the "right" single

failure along with the maximum temperature or minimum level conditions. The team

reviewed this finding in accordance with IMC 0609, "Significance Determination

Process. The finding screened as Green in the SDP Phase 1, since this issue was a

design deficiency that would not likely result in the loss of function per Generic Letter

(GL) 91-18, Revision 1. Therefore, the issue was determined to have a very low safety

significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, as of August 29, 2003, the ultimate heat sink maximum

temperature and minimum level design basis, as described in the USAR had not been

correctly translated into a specification. Specifically, the USAR described a limiting

single failure for both the maximum temperature and minimum level condition, and the

design basis calculations did not address the time necessary for the operators to

recover from the single failure.

This issue was entered into the licensee's CAP as CRs 02-05372, 02-05986, 02-06337,

03-06507, and 03-07042. Because this issue was of very low safety significance and

because it was entered into the licensees CAP, this violation is being treated as a NCV

consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000346/2003010-17).

.14 Auxiliary Feedwater System Calculation Issues With Main Steam Safety Valves

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to ensure

that design analyses showed that the AFW system could perform its safety function

under design basis conditions. Following discovery, the licensee entered the issue into

its corrective action system. The primary cause of this violation was related to the

cross-cutting area of human performance, as the licensee used the results of a vendor

calculation without verifying that it was adequate.

Description: The team reviewed CR 02-07236 and the licensees calculation

C-NSA-050.03-013 for AFW system hydraulic characteristics, which included calculating

the hydraulic resistance of flow to the steam generators. When determining the

hydraulic system resistance, it was noted that the calculation did not consider the

increased backpressure caused by allowable MSSV drift and safety valve accumulation.

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This could have a negative affect on analyzed AFW pump flow because the higher

backpressure would decrease AFW flow to the steam generators and reduce heat

removal capability for the AFW system. In resolving this issue, the licensee reviewed

the loss of feedwater analysis of record, 32-1171148-00, and determined that the MSSV

drift and accumulation had not been considered in this vendor calculation. The vendor

calculation was used as an input to calculation C-NSA-050.03-013 for determining the

AFW system resistance curve. Since the vendor calculation was in error, the licensees

calculation was in error as well.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to assess the effect of increased back pressure in the AFW system.

Since there was a performance deficiency, the team compared this performance

deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC

0612, "Power Reactor Inspection Reports." The team concluded that the issue was more

than minor because the calculations were non-conservative and because the calculation

of record did not demonstrate that the AFW system could perform its safety function

under design basis conditions. Based on further analysis, the licensee concluded the

AFW system was operable. This was a design issue which affected the mitigating

systems cornerstone. The team reviewed this finding in accordance with IMC 0609,

"Significance Determination Process, and answered no to all five screening questions

in the Phase 1 Screening Worksheet under the Mitigating Systems column. The team

concluded the issue was of very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to implement effective design control

measures to check and verify the adequacy of the design basis calculation performed by

the vendor of the AFW system hydraulic analyses for all postulated accidents. This

issue negatively reflected on the adequacy of the licensees oversight of the engineering

contractor performing the calculations. The licensee entered the issue into its CAP as

CR 03-02651. Because this issue was of very low safety significance and because it

was entered into the licensees CAP, this violation is being treated as a NCV, consistent

with Section VI.A.1 of the NRC Enforcement Policy. (NCV 05000346/2003010-18)

.15 Auxiliary Feedwater Strainer Mesh Size and Preconditioning of Auxiliary

Feedwater System During Testing

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XI,

having very low safety significance (Green). Specifically, the licensee failed to

recognize that flushing the system and blowing down the strainers upstream of the

turbine driven pump bearing cooling water strainers prior to routine surveillances

constituted preconditioning of the AFW system. Following discovery, the licensee

entered the preconditioning issue into the corrective action program. The primary cause

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of this violation was related to the cross-cutting area of problem identification and

resolution, because the licensee had failed to recognize the consequences of the

preconditioning when evaluating an earlier issue and determining that a larger mesh

size could be installed in the strainers.

Description: The licensee designated CR 02-04673 as a SCAQ CR which described

discovery that the strainers in the SW supply to the turbine driven pump bearings had a

smaller mesh size than that of the main SW strainers. It also addressed the possibility

of blockage of the restricting orifices in the AFW system due to debris within the SW

system. The following CRs were rolled into CR 02-04673: 02-05639 and 02-06861.

Both an operability evaluation and a root cause report were required for CR 02-04673.

In addition, an engineering change package was initiated to add new strainers upstream

of the restricting orifices and to increase the mesh size in the existing strainers.

OPERABILITY DETERMINATION: Because the licensee had extensively cleaned the SW

system piping during the outage, the team did not disagree with the conclusion reached

in the operability determination that the AFW system was operable. However, the

following non-conservatisms in the analysis were noted:

The operability determination assumed that the AFW system would run on

minimum recirculation flow until all of the SW in the "dead leg" leading to the

pumps has passed through the lines. However, under the postulated seismic

event causing a loss of offsite power (LOOP), AFW would be required to function

since the main feedwater pumps would be unavailable. The accident analysis

assumed that AFW flow to the steam generators would be supplied within

60 seconds. The starting sequence for the pumps would have the flow

immediately being directed through the pumps and into the steam generators.

In the short term, 100 percent of the AFW flow would be directed into the steam

generators. Only after a period of time would the pumps be throttled back or the

recirculation lines opened to divert water. Therefore, the team did not agree that

this assumption was reasonable. Furthermore, it appeared that the licensees

analysis had not considered the actual design basis for the system.

The operability determination noted that the bearing strainers had not shown any

sign of clogging during periodic testing with SW. However, the licensee failed to

note that this was because the procedures required the line to be flushed and

the strainers to be blown down prior to and after each test, thus eliminating the

potential for any clogging.

ROOT CAUSE REPORT: The licensee issued a root cause analysis in March 2003 which

determined the cause of the limiting particle size for the AFW strainers. At that time, the

licensee's CAP did not require use of a formal root cause process. Therefore, even

though the issue was determined to be a SCAQ, the licensee did not determine the root

cause because the issue was, as stated in the root cause report, "historical." The team

ascertained that because the root cause report did not follow a formalized process, the

report was actually more like an apparent cause analysis than a root cause evaluation.

Similar to the operability determination, the cause evaluation noted that the strainers to

the coolers were periodically flushed and blown down during testing. However, the

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evaluation failed to recognize that this constituted preconditioning of the test. The report

did not evaluate the beneficial impact that the pre-test flushing and strainer blowdown

would have in regard to required maintenance of the coolers.

The modification history developed in the cause evaluation showed that the licensee

had significantly increased the strainer mesh sizes in 1985 without discussion of the

bearing oil cooler strainers. However, the evaluation did not address whether these

modifications resulted in changes to the testing procedures, such as the currently

imposed pre and post test flushing and strainer blowdown.

The evaluation did not address whether the cooler for the pump bearings could handle

the increased particle size. There was no documentation in the evaluation which

addressed the acceptability of the increased strainer mesh size on the components

which the strainer was designed to protect. Although the evaluation discussed the need

for operator attention to an alarm for a blocked strainer, it did not recognize that the

larger particles could cause blockage of a downstream component that could not be

cleared by back-washing of the strainer.

ENGINEERING CHANGE PACKAGE: The engineering change package, ECR 03-0074,

stated that a conceptual design was not necessary due to the simplicity of the design

and the great deal of study that went into producing the initiation report. The package

acknowledged that the strainers were in the lines which supply cooling water to the

pump and turbine bearing oil coolers, the turbine governor oil cooler and the pump

mechanical seals. However, it did not discuss why the increased strainer size would not

affect any of these components.

In response to the teams questions, the licensee provided the team with a vendor

manual which contained a single line which stated that the bearing oil coolers had

openings greater than 0.0625 inches such that they could handle the larger size

particles if the strainer mesh size was increased. The licensee engineers stated these

coolers were the limiting components. However, this information was not documented

and there was no evidence that the licensee had considered this information prior to the

team's questions.

Further discussions with the licensee determined that the bearing oil coolers had never

been opened for inspections and were not included in the GL 89-13 heat exchanger

program. The team concluded this had not been a problem in the past because of the

very small mesh strainer. The licensee wrote CR 03-06576 to address this issue.

Nonetheless, the team concluded that the modification was a work in progress as it had

not been implemented by the end of the inspection.

REVIEW OF PERIODIC TEST PROCEDURE: As discussed above, the issue of flushing the

lines and blowing down the strainers both prior to and following a periodic surveillance

was reviewed by the team. This issue was raised based on a review of periodic

procedure DB-SP-04152, which used SW as the source of cooling water for the test

duration. The licensee investigated the issue and determined that other AFW

surveillance tests also flushed the lines and blew down the strainers prior to the test

being performed. The team determined that the flushing of the lines blowing down of

the strainers constituted pre-conditioning of the turbine driven AFW pumps because it

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masked any performance problems which could occur during an actual event. The

availability and reliability of the system was intended to be ensured through the periodic

testing. The team noted that the licensee had stated that no problems with the strainers

had occurred as part of the justification for increasing the strainer mesh size. However,

the team concluded that the licensees procedural actions would have masked any

problems. A violation of NRC requirements was identified.

Analysis: The team determined that a performance deficiency existed because the

licensees practice, as prescribed in site procedures, prevented the AFW system from

being tested in its as-found condition. Since there was a performance deficiency, the

team compared this performance deficiency to the minor questions contained in

Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The

team concluded that the issue was more than minor because there was not sufficient

information to demonstrate that test requirements would have been met had the

strainers not been blown down. This was a procedural issue which affected the

mitigating systems cornerstone. Because the licensee's practices prevented a true

assessment of previous operability, the team could not determine if the turbine driven

pumps would have been inoperable if the strainers were not blown down. However,

discussions with the licensee did not indicate that a large amount of material was seen

during the system flushes and strainer blowdowns. Therefore, the licensee considered

the system to be operable. The team reviewed this finding in accordance with IMC

0609, "Significance Determination Process, and answered no to all five screening

questions in the Phase 1 Screening Worksheet under the Mitigating Systems column.

The team concluded the issue was of very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XI requires, in part, that a test

program be established to demonstrate that components will perform satisfactorily in

service. Contrary to the above, as of September 29, 2003, the test procedures for the

AFW turbine high speed stop and overspeed trip did not demonstrate that the system

would perform satisfactorily in service because the test included a step to flush the

cooling water lines and blow down the strainers prior to performing the test. These

actions prevented any adverse effects due to strainer blockage from being discovered.

Failure to adequately test the system was a violation of Appendix B, Criterion XI. This

issue has been entered into the licensee's CAP as CR 03-06520. This violation is being

treated as a NCV consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000346/2003010-19)

.16 Inadequate Evaluation of System Health Condition Report on Auxiliary Feedwater

Design Bases Calculations

Introduction: The team identified a performance deficiency involving the licensee's

failure to adequately evaluate a condition report written as part of the licensee's internal

system health assessment. Following discovery, the licensee made corrections to the

existing condition report evaluation. This was a minor violation.

Description: During review of CR 02-05904, the team identified that the cause

evaluation was not adequately performed. This CR addressed a system health report

issue on whether certain AFW design basis calculations existed or were outdated. The

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evaluation determined that all the questioned calculations did exist and that no further

action was needed. The following deficiencies in the evaluation were identified:

The evaluation listed an incorrect calculation number and an incorrect revision

for another calculation.

The evaluation identified a calculation for maximum steam pressure in the AFW

system; however, it failed to recognize that the calculation was incorrect (this

issue is discussed in Section 4OA3(3)b.14).

The evaluation stated that CR 02-06356 identified the causes for the condition;

therefore, no additional action needed to be taken. However, CR 02-06356,

which had been evaluated three months prior to CR 02-05904, did not actually

identify the causes, but rather assumed that the causes were known and that all

appropriate corrective actions had been identified (this issue is discussed in

Section 4OA3(3)b.22).

Analysis: The team determined that a performance deficiency existed because the

licensee failed to evaluate a condition adverse to quality regarding calculations on the

AFW system. Since there was a performance deficiency, the team compared this

performance deficiency to the minor questions contained in Appendix B, "Issue

Screening," of IMC 0612, "Power Reactor Inspection Reports." Because the team

independently identified the deficiencies which the licensee had failed to assess, the

failure to properly evaluate an identified condition adverse to quality had no safety

impact. Therefore, the team concluded this performance deficiency was minor.

Enforcement: The failure to perform an adequate cause evaluation for a condition

adverse to quality constitutes a violation of 10 CFR Part 50, Appendix B, Criterion XVI,

which has minor significance and is not subject to enforcement action in accordance with

Section IV of the NRCs Enforcement Policy.

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case due to the licensee's

inadequate evaluation. Additionally, the underlying cause is similar to that of other

findings in this report.

.17 Containment Post-LOCA Trisodium Phosphate

Introduction: The team identified a performance deficiency involving the licensee failing

to approve a calculation prior to relying on the results of the calculation. The calculation

addressed the capability of the TSP in baskets in the lower level of containment to

control the pH of sump water following a postulated design basis accident. Following

discovery, the licensee entered the issue into its corrective action program and

approved and issued the calculation.

Description: The team reviewed CRs 02-02943, 02-05300 and 02-05304. These CRs

questioned the adequacy of the TSP design from three aspects:

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Capability of the TSP baskets to perform their function in light of a new

calculation for containment flood level which revealed that the baskets would not

be fully submerged;

Two different calculations provided conflicting conclusion regarding the time

when sump pH would be greater than 7.0; and

Whether the amount of TSP in the baskets was sufficient to neutralize sump

water with acidification from other post-LOCA sources such as degraded

coatings and insulation.

Concerns were also raised regarding the impact of the additional boric acid in the

containment during the previous operating cycle on the capability of the TSP baskets to

fulfill its safety function.

The licensee addressed the concerns of all three CRs through the corrective actions

specified for CR 02-05300. Re-analysis of the containment flood level and the TSP

basket contents was performed in calculations C-NSA-059.01-019 and 86-5024418-01.

These calculations demonstrated that, with the recalculated flood level, the amount of

TSP in the baskets was sufficient to meet the sump pH-control requirements of the

USAR. Analysis of the impact of the additional boric acid inside the containment was

performed in calculation C-NSA-040.01-006. This calculation evaluated the amount of

TSP needed to neutralize the boric acid deposited in the containment from a variety of

RCS leakage scenarios, including RCS unidentified leakage over the previous three

operating cycles plus the boric acid deposited as the result of head leakage. This

calculation demonstrated that for the identified level of leakage, with the amount of boric

acid deposited from the head leakage (conservatively assumed to be entirely dissolved

into the sump), the TS required amount of TSP would neutralize all of the boric acid.

The team found the issue difficult to evaluate as a result of the number of rollovers

involved in the resolution of these issues. The issues were ultimately consolidated into

three corrective actions under CR 02-05300; all three corrective actions involved the

completion of vendor calculation 86-5024418-01. The team determined that the three

corrective actions had been marked as completed although one calculation had not

been approved and had, in fact, been remanded to the vendor for revisions. This was

not in accordance with the licensees CAP procedure. Specifically, procedure

NOP-LP-2001, Condition Report Process, Revisions 3 and 4, required that corrective

actions be completed prior to the corrective action being accepted and closed. The

revisions to the calculation were determined to be minor and did not affect the results,

and the licensee formally approved the calculation. The team did not review the final

calculation results.

The team determined that a performance deficiency existed because the issue involved

the licensees failure to approve a calculation prior to relying on the results of the

calculation and this issue was not identified during the corrective action closure process.

Since there was a performance deficiency, the team compared this performance

deficiency to the minor questions contained in Appendix B, "Issue Screening," of IMC

0612, "Power Reactor Inspection Reports." The team concluded that the performance

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deficiency was minor because the changes to the unapproved calculation were minor

and did not affect the overall results.

Enforcement: The closure of all the corrective actions for CR 02-05300, contingent upon

completion of vendor calculation 86-50244181-01, which had not been owner accepted,

was considered a violation of 10 CFR Appendix B, Criterion V, which has minor

significance and is not subject to enforcement action in accordance with Section IV of

the NRCs Enforcement Policy. The licensee entered the issue into its CAP as

CR 03-07420.

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case due to the rollover issues

which were identified and the underlying cause is similar to that of other findings in this

report.

.18 Borated Water Storage Tank Calculation Issues

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance. Specifically, the licensee failed to translate the

radiological consequences of leakage from engineered safety feature components

outside containment into calculations of record for post-accident control room dose and

offsite boundary dose. Following discovery, the licensee entered the issue into its

corrective action program and provided a bounding evaluation which demonstrated that

the increase in dose was within acceptable limits.

Description: During the SSDI, the NRC identified that the radiological consequences of

leakage from engineered safety features components outside the containment were not

included in the calculation of offsite dose for 10 CFR Part 100 nor in the calculation for

control room dose per GDC 19. The concerns involved the impact on control room dose

as a result of an airborne release from the assumed 500 gallons of containment sump

water deposited in the BWST and the impact on both offsite and control room dose as a

result of ECCS system pump seal leakage. The licensee wrote CRs 02-06701,

02-07713, and 02-07701 to address these issues.

The licensee performed an informal calculation in the cause analysis for CR 02-07701 to

determine the increase in dose in the control room from the 500 gallons deposited in the

BWST. The calculation was based on the site boundary base dose listed in the USAR

which resulted from the airborne release associated with the 500 gallons of post-LOCA

water deposited in the BWST. This dose was determined by the Bechtel calculation of

record as 2.72 rem. Using control room ventilation system parameters and the site

boundary dose, the control room dose was calculated as 0.07 rem. The licensee

extrapolated the dose for the 40 gallon per hour pump seal leakage from the USAR

dose rate for normal valve system leakage of 5890 cubic centimeters per hour (1.56

gallons per hour). The result was an additional control room dose of 0.5 rem and an

additional site boundary dose of 1.5 rem.

The licensee then calculated that the total offsite dose, resulting from the USAR value of

232 rem accident dose plus the BWST dose of 2.72 rem plus the pump seal dose of

1.5 rem, was a total of 236.22 rem. The total control room dose was similarly summed:

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USAR accident dose of 19.8 rem plus BWST dose of 0.066 rem plus pump seal leak

dose of 0.5 rem for a total of 20.366 rem.

As a result of these calculations, the licensee specified post-restart corrective actions to

update the Bechtel calculation of record and the USAR to incorporate these doses.

Because the corrective actions had not yet been completed, the licensee had not

completed a screening or evaluation under 10 CFR 50.59. The team performed a

limited evaluation of the acceptability of the increased dose under 10 CFR

50.59(c)(2)(iii), "Result in more than a minimal increase in the consequences of an

accident previously evaluated in the final safety analysis report (as updated)." The team

reviewed the guidance provided in Nuclear Energy Institute (NEI) standard 96-07,

"Guidelines for 10 CFR 50.59 Implementation," Revision 1, which NRC endorsed in

Regulatory Guide 1.187.

Based on this guidance, the team determined the revised dose calculations did not

result in more than a minimal increase in the consequences of an accident previously

evaluated in the USAR. The team determined that a more than minimal increase would

have occurred if:

The increase in dose was more than or equal to ten percent of the difference

between the previously calculated dose value and the regulatory guideline value

(10 CFR Part 100 or GDC 19); and

The increased dose exceeded the current standard review plan guideline value

for the particular design basis event.

The team calculated that ten percent of the difference between the previously calculated

dose total and the 10 CFR Part 100 and GDC 19 limits were 6.8 rem for the offsite dose

increase and 1.02 rem for the control room dose. The team confirmed that the total

increases in dose of 4.2 and 0.57 rem were below the guidance values in NEI 96-07;

therefore, the first part of the guidance was satisfied. The team concluded that the

second part of the guidance was met because the total offsite dose was less than the

Part 100 limit of 300 rem and the control room dose was less than the GDC 19 limit of

30 rem. The team, therefore, deemed that the licensee had an acceptable rationale for

delaying issuance of the formal calculations until after restart.

Analysis: The team determined that a performance deficiency existed because the

licensee had not recognized that the radiological consequences of leakage from

engineered safety features components outside the containment were not included in

the calculation of offsite dose for 10 CFR Part 100 nor in the calculation for control room

dose per GDC 19. Since there was a performance deficiency, the team compared this

performance deficiency to the minor questions contained in Appendix B, "Issue

Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded

that the issue was more than minor because the licensee had to perform calculations to

show that the increased doses remained within the post accident dose level

requirements.

The team reviewed the SDP questions for reactor safety, occupation radiation safety

and public radiation safety contained in MC 0612, Appendix B, Issue Screening, and

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also consulted with the senior reactor analysts (SRAs). Based on this review, the team

determined that the issue was not covered by any of the revised oversight cornerstones

and was, therefore, not suitable for SDP analysis. This determination was based on the

issue being a design issue that dealt with postulated doses following a design basis

accident. The team also determined that the increase in dose did not involve an issue

requiring a license amendment. Therefore, this finding was reviewed by Regional

Management, in accordance with IMC 0612. The finding was determined to be of very

low safety significance (Green) because the preliminary calculations concluded that the

increased doses remained within the post accident dose level requirements and there

were no actual releases.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to translate the radiological consequences of

leakage from engineered safety feature (ESF) components outside containment into

calculations of record for post-LOCA control room dose and offsite boundary dose.

The licensee entered the issue into its CAP as CRs 02-06701, 02-07713, and 02-07701.

Because this violation was of very low safety significance and because it was entered

into the licensees CAP, this violation is being treated as a NCV consistent with

Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-20)

.19 Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover Stud

Overstressing

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance. Specifically, the licensee failed to evaluate a

potential overstressing condition on the reactor coolant pump casing-to-cover studs.

Following discovery, the licensee entered the issue into its corrective action program.

The primary cause of this violation was related to the cross-cutting area of problem

identification and resolution as the licensee closed a condition report without recognizing

that the apparent condition adverse to quality had not been addressed.

Description: The team reviewed CR 02-08759. This CR questioned whether the RCP

casing-to-cover studs had been overstressed when the studs on all four pumps were

retensioned in 1996. The RCP casing-to-cover studs are part of the reactor coolant

pressure boundary (RCPB).

The team identified the following deficiencies with the licensees handling of this CR:

The CR was closed based on a draft revision of a vendor calculation, SR-0964,

Revision 1, which was not accepted by the licensee until after the CR was

closed.

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The discrepant condition (possible overstressing of the studs) was neither

analyzed as not being a concern nor field verified to not be a problem before the

CR was closed. Instead the corrective action was canceled on the basis that the

studs on pumps 1-1 and 1-2 had relaxed to within acceptable limits, therefore,

the studs on the other two pumps were also deemed acceptable.

The draft calculation only addressed the allowable stud tension for pumps 1-1

and 1-2, based on the new gaskets installed; it did not address the condition

from 1996 for all four pumps or the continuing condition on pumps 2-1 and 2-2.

When questioned by the NRC team the licensee had to go back to the vendor

and obtain a new calculation to show that the previous stud elongation was

acceptable. However, no new CR was written to address the fact that 02-08759

had been closed without addressing the concern for which it had been written.

Instead of being provided with a new calculation, the vendor provided the

licensee with a letter providing the maximum allowable stud elongation for the

1996 configuration.

The actual 1996 as-left elongation values for some of the studs were greater

than the 24 mils specified in the vendor letter, although they were within the 26

mils specified in 1996. The licensee verbally evaluated the condition, but did not

actually document the acceptability of the 1996 condition.

The vendor letter was appended to the CR file four months after the CR was

closed and only after the team questioned why no CR was written about the

issue.

Because of this sequence of events, the team performed a limited, independent

verification of both the formal and informal calculation results, and then verified the

actual installed stud elongation against the calculated allowable. The team determined

that some studs were elongated to 25 mils; however, the quadrant average in all cases

was between 23.2 and 23.4 mils. The team determined that an average elongation of

24.3 mils would keep the stress levels below the maximum American Society of

Mechanical Engineers (ASME) boiler and pressure vessel code (the Code) allowable of

23.6 kilo-pounds per square inch (ksi). Based on this independent evaluation, the team

concluded that the casing-to-cover studs on RCPs 2-1 and 2-2 were not overstressed

and that none of the studs on any of the four RCPs not been overstressed in the past.

The team also noted that the licensee did not have a design basis calculation that

supported the increased tensioning of the studs on all four reactor pumps in 1996 and

still did not have such a calculation for RCPs 2-1 and 2-2 in 2003. However, the

licensee planned to replace the gaskets on these pumps by no later than RFO 14 in

2005; once the gaskets are replaced, the stud tensioning would be addressed by

calculation SR-0964.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to evaluate the acceptability of the RCP studs prior to closing the CR.

Additionally, when the issue was brought to their attention, the licensee did not write a

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new CR to document the failure of the CAP. Since there was a performance deficiency,

the team compared this performance deficiency to the minor questions contained in

Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The

team concluded that the issue was more than minor because the licensee had to

perform calculations to determine if the RCP studs were within ASME Code allowables.

The team reviewed this finding in accordance with IMC 0609, "Significance

Determination Process. The team assessed the finding through Phase 1 of the SDP.

The issue involved the barrier integrity cornerstone because it dealt with the

acceptability of the RCPB. There was only one question related to the RCPB. The

licensee had not evaluated the functionality of RCP studs for past operation or for

current operation on two of the four pumps. Therefore, the team assessed the issue

based on the team's evaluation described above. Based on this assessment, the RCP

studs were always functional and the SDP RCPB question was answered as "no".

Therefore, the finding screened out as having very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, in March 2003, the licensee closed CR 02-08759 without

ensuring that the ASME Code requirements were correctly translated into the torquing

values for the RCP casing-to-cover studs and without ensuring that previous

maintenance activities had not resulted in the studs being overstressed.

After being identified as a potential violation at the end of the inspection, the licensee

wrote CR 03-07047 to enter the issue into the CAP. Since the issue was of very low

safety significance and was captured in the licensee's CAP, it is being treated as a NCV,

consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000346/2003010-21)

.20 Reactor Coolant Pump Inner Gasket Leakage

The team reviewed CRs 02-01523, 02-03668, and 03-04018, and associated

evaluations, which documented an apparent continuing problem with RCP inner gasket

leakage. The team determined that the licensee failed to adequately analyze the results

of an apparent continuing leak past the inner gasket on the RCPs. Specifically, minor

leakage past the inner gasket was noted on all four pumps during previous outages and

the documented evaluation did not address why it was acceptable to not repair the

gaskets. Furthermore, the licensee's analysis did not provide technical justification for

either replacing or not replacing all four RCP gaskets.

The team performed extensive evaluation of the as-left leakages for all pumps by

reviewing test results and test log books. The responsible test engineers were also

interviewed by the team. The team determined that the licensees evaluations were

based on leak testing that: (1) did not use the same methodology from outage to

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outage; (2) did not attempt to normalize the data from outage to outage; (3) did not

consider the impact of reactor coolant pressure and temperature conditions on the test

results; and (4) was only intended to verify that the leak detection lines were open and

not blocked. The team was concerned that the licensee did not recognize these

inconsistencies in performing and approving the evaluation.

The team determined that the design of both the inner and outer gaskets was to seal

against full reactor pressure. While normally the inner gasket provided the seal, the

outer gaskets was also designed for this purpose. Only if the outer gasket failed would

the RCPB, provided by the casing-to-cover studs, be affected.

The team also noted that leakage past either the inner or outer gasket was not pressure

boundary leakage, per the ASME Code. The Code specifically excluded gaskets from

RCPB leakage. Instead, any leakage past the outer gasket would be categorized as

either identified or unidentified reactor coolant leakage, and would be subject to TS

limits. Leakage past the inner gasket was not considered to be a safety concern.

Neither the inner or the outer gasket was considered to be important to safety and

neither component was credited with having a safety function in the USAR.

The team determined that a catastrophic failure of the inner gasket during an

operational cycle should have no consequences, as the outer gasket should continue to

provide a seal. If the outer gasket also failed, then the licensee would have to comply

with the TS limiting conditions for operation and shut down the plant.

The team noted that the normal operating pressure and temperature (NOP/NOT) test

performed by the licensee included inspections of the RCPs: both at the gasket leakoff

lines and at the studs. These inspections were conducted prior to, during and following

reaching NOP/NOT. This NOP/NOT test showed that there was no outer gasket

leakage and that the inner gasket leakage was minor, occurred primarily during the

pressurization period and stopped, or significantly slowed, once the pumps reached an

equilibrium temperature.

Notwithstanding that the licensee failed to adequately analyze the results of an apparent

continuing leak past the inner gasket on the RCPs, the team concluded that this did not

present a safety issue since the inner gasket leakage would not affect the RCPB. No

violation of NRC requirements were identified.

.21 Environmental Qualification of Equipment Not Supported by Analysis

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,

having very low safety significance (Green). Specifically, the licensee failed to ensure

that emergency core cooling system pump motors were environmentally qualified for the

stated mission time, as stated in a license amendment request (LAR) submitted to the

NRC. Following discovery, the licensee entered the issue into its corrective action

program. The primary cause of this violation was related to the cross-cutting area of

human performance as the licensee did not ensure that personnel developing license

documents had the necessary information.

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Description: The team examined CR 02-05732, which was issued during the licensees

latent issues review of the SW system. The fundamental concern discussed in the CR

was that LAR 96-0008, submitted to NRC by the licensee on July 28, 1999, contained

statements that were unsupported by analyses.

The CR identified three specific concerns:

Some equipment in the ECCS pump rooms was not qualified to higher

temperatures, as stated in the request;

There was no analysis to support a statement in the request that two room

coolers were adequate even with substantially degraded flow rates; and

The request stated that no changes were made in AFW flow, yet a calculation of

record showed that the flow rate was changed from 1600 gpm to 800 gpm.

The team reviewed the condition description, immediate actions, and cause analysis.

The cause analysis examined the three concerns and concluded that there was no

discrepant condition, no apparent cause, and no corrective actions required.

The team disagreed with this conclusion based on a review of CR 02-05593 which

identified a block of components that were not included in a calculation evaluating

environmental qualification (EQ) qualification of equipment in the ECCS pump rooms.

This CR also noted that no reference for qualification of the HPI and DHR pump motors

existed and recommended that the EQ calculation be revised to address qualification of

all these components.

The team identified that the first concern in CR 02-05732 was correct, in that two pieces

of equipment in an ECCS pump room, the containment spray (CS) and HPI pump

motors, were not environmentally qualified for the service time of 30 days which was

stated in the LAR. Based on a review of the EQ folder, the team determined that the

motors could most likely be qualified as required. CR 03-06588 was written to address

this issue. However, the team later determined that the licensee had evaluated

CR 03-06588 and concluded that no corrective actions needed to be taken as far as

environmentally qualifying the ECCS motors.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to establish the environmental qualification of two ECCS motors at the

time the license amendment request was submitted. Since there was a performance

deficiency, the team compared this performance deficiency to the minor questions

contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports." The team concluded that the failure to adequately evaluate the motor

environmental qualification issue was more than minor because it reflected a weakness

in the licensees CAP in regard to correctly assessing issues. The team concluded that,

if uncorrected, this continuing weakness could result in a repeat failure of the CAP to

adequately identify, evaluate and correct problems. This was an equipment qualification

issue which affected the mitigating systems cornerstone. Although the licensee had not

qualified the equipment, the team deemed that the motors more likely than not could be

qualified. Therefore, the team considered it reasonable that the motors would perform

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their safety function, if required to operate. The team reviewed this finding in

accordance with IMC 0609, "Significance Determination Process. The finding was

screened in the SDP Phase 1 as a qualification deficiency that was confirmed not to

result in the loss of function per Generic Letter 91-18, Revision 1. Therefore, the issue

was determined to have a very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that

conditions adverse to quality be promptly identified and corrected, commensurate with

their safety significance.

Contrary to the above, in November 2003, the licensee evaluated CR 03-06588, which

described a condition adverse to quality, and concluded that no corrective actions were

necessary. The condition adverse to quality described in the CR dealt with LAR 96-008

which documented that the HPI and DHR pump motors were environmentally qualified

for 30 days, when, in fact, those motors were not so qualified.

After being identified as a potential violation at the end of the inspection, the licensee

wrote CR 03-06588 to enter the issue into the CAP. Since the issue was of very low

safety significance and was captured in the licensee's CAP, it is being treated as a NCV,

consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000346/2003010-22)

.22 Inadequate Justification for Downgrade of Significant Condition Adverse to

Quality

Introduction: The team identified a performance deficiency involving the licensee's

failure to evaluate an issue initially determined to be a significant condition adverse to

quality prior to downgrading the issue. Following discovery, the licensee entered the

issue into its corrective action program. This was a minor violation.

Description: Prior to the safety system design inspection in October 2002, and following

completion of the system health reviews, the licensee initiated CR 02-06356 to

document a repetitive concern regarding a difficulty in determining the status or location

of design basis calculations. This CR was determined to be a SCAQ, primarily because

a number of design basis calculations were discovered to be outdated or non-existent.

Issues such as those discussed in Section 4OA3(3)b.16 exemplified the reason that the

CR originally was rated as a significant condition.

The team reviewed CR 02-06356 and noted that it had been downgraded to a routine

CR with minimal investigation or justification. The evaluator assumed that his

department had the bulk of the calculations and that he knew the status of those

calculations. The evaluator then concluded that there was not really a problem, based

on these assumptions and apparently without considering other design engineering

departments. Additionally, the team determined that the extent of condition review was

based entirely on a word search for the word "calculation" in the title of CRs. This

eliminated many of the CRs written on superceded or historical calculations and resulted

in many of the CRs on design basis calculational issues not being found.

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Analysis: The team determined that a performance deficiency existed because the

licensee failed to adequately assess and justify the downgrade of a condition adverse to

quality as required by procedure NOP-LP-2001. Since there was a performance

deficiency, the team compared this performance deficiency to the minor questions

contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor Inspection

Reports." The team concluded that the performance deficiency was minor because the

team did not identify other examples where downgrades were performed without

adequate justification and because no specific calculation deficiencies which resulted in

inoperable equipment were associated with the CR.

Enforcement: The failure to provide adequate justification when downgrading a SCAQ

constitutes a violation of 10 CFR Part 50, Appendix B, Criterion V. However, this

violation was determined to have minor significance and is not subject to enforcement

action in accordance with Section IV of the NRCs Enforcement Policy. The licensee

documented the issue in CR 03-06948.

While minor violations are not normally documented in inspection reports, the team

determined that documentation was appropriate in this case due the underlying cause is

similar to that of other findings in this report.

.23 Inappropriate Application of 10 CFR 50.59

Introduction: The team identified a NCV of 10 CFR 50.59, Changes, Tests and

Experiments. Specifically, the licensee failed to preform an adequate evaluation of a

defacto modification to the plant where the underlying change may have required NRC

approval prior to implementation. Following discovery, the licensee entered the issue

into its corrective action program and re-performed the evaluation; the licensee also

repaired those barriers which were physically degraded. The primary cause of this

violation was related to the cross-cutting area of human performance as the licensee

appeared to selectively choosing information from the guidance document.

Description: In IR 05000346/2002019, LER 05000346/2002-006 was closed and an URI

was opened to track resolution of safety related structures which were unprotected

against tornado missiles; specifically that six feet of the EDG exhaust stacks were

unprotected and that portions of a concrete barrier were degraded. This issue was

being tracked in the licensee's corrective action system under CRs 02-04146, 02-04147,

02-04700 and 02-05590. The team determined that the licensee had evaluated the

non-conforming conditions using a computer code (TORMIS) discussed in Electric

Power Research Institute (EPRI) Topical Report NP-2005, "Tornado Missile Risk

Evaluation Methodology," Volumes I and II, August 1981. Based on use of this code,

the licensee determined the probability of the unprotected areas being struck by a

tornado missile was relatively low.

The licensee revised the USAR to incorporate the TORMIS methodology, including a

provision which allowed it to be used to accept degraded or non-conforming conditions.

On that basis, the licensee declared the diesel generators operable and determined that

repairs were not needed for the non-conforming structures until 2004. In regard to the

unprotected stacks, the licensee determined that no modifications were necessary.

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Prior to the USAR change, Section 3.5.1 of the USAR stated that, "Protection against a

potential missile may be provided by, but not necessarily limited to, any one or

combination of the following protection methods: compartmentalization, barriers,

separation, distance, restraints, strategic orientation and equipment design." The team

noted that all these methods involved physical protection of the equipment, rather than

methods of evaluation. Under change notice 02-063, the licensee changed this

statement to add tornado missile probability as a protection method.

As part of the USAR change, the licensee performed an evaluation as required by

10 CFR 50.59. During review of this evaluation, the team questioned whether the

licensee had appropriately followed the guidance in Nuclear Energy Institute standard

NEI 96-07, which NRC endorsed in Regulatory Guide 1.187. Specifically, the licensee

appeared to be incorporating use of the TORMIS methodology, using the methodology

to accept a defacto change to the plant (where the plant did not match the description in

the USAR) and then justifying the methodologys use for future non-conforming or

degraded conditions all in the same 50.59 evaluation. The team noted that these

differing applications affected how the 10 CFR 50.59, Section c.2, questions were

answered in the licensees 10 CFR 50.59 evaluation. The team also noted that the

questions were answered based on the standard review plan, rather than on the

Davis-Besse USAR.

The team consulted with the Office of Nuclear Reactor Regulation (NRR) and

determined that the licensee should have evaluated the change from protecting

equipment from tornado generated missiles by means of physical protection to relying

upon analysis to demonstrate that such protection was not needed through use of a

probabilistic computer methodology.

In discussions, the licensee stated that the above approach was not necessary because

the TORMIS methodology was an "approved methodology and, therefore, wasnt a

departure from a method of evaluation described in the FSAR (as updated) used in

establishing the design bases or in the safety analyses" as defined in 10 CFR 50.59.

However, the team noted that there was not an existing method of evaluation that

applied to protection of the EDGs. Instead, the change was from "protection by means

of a physical barrier," to "protection by means of a probabilistic approach," which

appeared to have introduced a new failure mode not previously evaluated for the EDGs.

The introduction of this new failure mode did not appear to be addressed by the

licensees 50.59 evaluation.

Specifically, the USAR previously stated that the diesel generators were not affected by

tornado generated missiles due to physical features. Inclusion of the TORMIS

methodology introduced the possibility that the diesels could be affected by tornado

generated missiles. The licensee answered this question in its 10 CFR 50.59 evaluation

by stating that "the probability of a tornado generated missile was incredible, that NRC

accepted use of probability for Davis-Besse in analyzing the probability that turbine

missile would penetrate containment, and by stating that the Davis-Besse acceptance

criteria was the same as that licensed at other plants."

However, the team noted the following guidance in NEI 96-07, Section 4.3.6:

"Malfunctions of SSCs are generally postulated as potential single failures to evaluate

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plant performance with the focus being on the result of the malfunction rather than the

cause or type of malfunction. A malfunction that involves an initiator or failure whose

effects are not bounded by those explicitly described in the USAR is a malfunction with a

different result..."

Based on this description, because possibility for the diesel generators to be damaged

by tornado missiles involved both an initiator and effects which were not bounded by

those explicitly described in the USAR, the team deemed that this question should have

been answered "yes" and prior NRC review of this change sought.

At the end of the inspection, the licensee had written a new CR, 03-06561, and was

revising the 10 CFR 50.59 evaluation to address the above issues. The revised 10 CFR

50.59 analysis was not reviewed by the team.

The team also noted that the licensee had to physically repair the degraded concrete to

restore its tornado protection capability. The licensee had not considered these physical

changes necessary until the team identified the concern regarding inappropriately using

10 CFR 50.59 to correct non-conforming or degraded conditions. However, new

physical barriers for tornado missile protection were not added to those areas which

initially lacked such barriers.

Analysis: This issue was determined to involve a performance deficiency because the

licensee misapplied the criteria of 10 CFR 50.59 and concluded that prior NRC approval

was not required when such a conclusion could not be supported by the documented

50.59 evaluation. Because violations of 10 CFR 50.59 are considered to be violations

that potentially impede or impact the regulatory process, they are dispositioned using

the traditional enforcement process instead of the SDP. Typically, the Severity Level

would be assigned after consideration of appropriate factors for the particular regulatory

process violation in accordance with the NRC Enforcement Policy. However, the SDP is

used, if applicable, in order to consider the associated risk significance of the finding

prior to assigning a severity level. Using IMC 0612, Appendix B, "Issue Screening," the

team determined that the finding was more than minor because physical barriers were

degraded or missing and because those barriers being degraded could result in one or

more of the diesel generators failing to fulfill their design function during a tornado. This

was a design issue which affected the mitigating systems cornerstone.

The team reviewed this finding in accordance with IMC 0609, "Significance Determination

Process. The consequence of the design was assessed through Phase 1 of the SDP.

The team answered the question, "Does this issue involve an actual loss of safety

function," as "Yes," because under a design basis tornado, the diesel generator exhaust

stacks were not physically protected. Based on this premise, the team entered Phase 2

of the SDP.

The team determined that the only event tree affected was LOOP concurrent with loss

of one EDG. This was based on the assumption that a tornado missile hitting both EDG

exhaust stacks would be an incredible event. The team decreased the initiating event

frequency from a "5" (once in 100,000 years) to a "3" (once in 1,000 years) based on the

fact that the Davis-Besse switchyard was struck by a tornado in 1998 (in this event,

EDG 1 did not start from the control room and was declared technically inoperable due

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to the room design basis temperature of 120F being exceeded). In reviewing the 1998

event, the team determined that one turbine driven AFW pump was out of service for

maintenance. Therefore, the team assumed that a turbine driven AFW pump was out of

service for purposes for the Phase 2 analysis. Based on these credible assumptions,

the technical issue was determined to have very low safety significance and the violation

is categorized as Severity Level IV.

Enforcement: Title 10 CFR 50.59(d)(1) requires that the licensees maintain records of

changes in the facility, of changes in procedures, and of tests and experiments made

pursuant to 10 CFR 50.59(c). It further requires that these records include a written

evaluation which provides the bases for the determination that the change, test or

experiment does not require a license amendment pursuant to 10 CFR 50.59(c)(2).

Contrary to the above, on November 7, 2002, the licensee approved a 50.59 evaluation

incorporating a change in the design basis to accept not physically protecting the EDG

exhaust stacks from tornado missiles. However, the evaluation did not provide the basis

for why a possibility for a malfunction of the diesel generators due to impact on the

diesel generator exhaust stacks by a tornado missile did not produce a different result

than any previously evaluated in the final safety analysis report.

The failure to provide a written evaluation which described the basis for concluding a

license amendment was not needed was a violation of 10 CFR 50.59(d)(1). This issue

has been entered into the licensees CAP as CR 03-06561. This Severity Level IV

violation is being treated as an NCV consistent with Section VI.A.1 of the NRC

Enforcement Policy. (NCV 05000346/2003010-23)

.24 Failure to Perform Comprehensive Moderate Energy Line Break Analysis

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to include

the environmental effects of a DHR pump seal failure in its moderate energy line break

analysis. Following discovery, the licensee entered the issue into its corrective action

program and performed the analysis.

Description: The licensee initiated CR 02-07757 to document the failure to perform a

comprehensive moderate energy line break analysis. This CR was rolled over into

CR 02-06370, which required that the concerns of additional heat generation caused by

the moderate energy line break (DHR pump seal) be addressed in the new calculation

being performed in response to CR 02-06370. The team determined that the heat load

caused by failure of the DHR pump seal (an additional 21,000 btu/hr) was included in

calculation C-NSA-032.02-006 and that the discrepant condition was adequately

resolved.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to have a design analysis to demonstrate the ability to withstand

moderate energy line breaks as specified in design documents. Since there was a

performance deficiency, the team compared this performance deficiency to the minor

questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor

Inspection Reports." The team concluded that the issue was more than minor because

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the licensee had to perform calculations to show that the environmental effects were

acceptable. This was a design issue which affected the mitigating systems cornerstone.

The team reviewed this finding in accordance with IMC 0609, "Significance

Determination Process, and, based on the determination that the moderate energy line

break heat loads were acceptable and that the system could perform its design function,

answered no to all five screening questions in the Phase 1 Screening Worksheet

under the Mitigating Systems column. The team concluded the issue was of very low

safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to translate the consequences of leakage from

the DHR pump seals into calculations of record for moderate energy line breaks. The

licensee entered the issue into its CAP as CRs 02-07757 and 02-06370. Because this

violation was of very low safety significance and because it was entered into the

licensees CAP, this violation is being treated as an NCV consistent with Section VI.A of

the NRC Enforcement Policy. (NCV 05000346/2003010-24)

(4)

Detailed Team Review of Licensee Corrective Actions Implemented to Address

Operational Issues Previously Identified by the Licensee

a.

Inspection Scope

The team assessed effectiveness of the licensees CAP to identify, categorize, evaluate,

and resolve the identified equipment, human performance or programmatic adverse to

quality plant conditions. The team mainly focused on plant systems design and

licensing basis requirements issues which were previously identified by the NRC, the

licensee and others during various design reviews conducted in 2002. The team

assessed effectiveness of the licensees corrective actions implemented to address

previously identified operational issues.

b.

Findings

Repetitive Spacer Grid Strap Damage

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVI,

having very low safety significance (Green). Specifically, the licensee failed to take

adequate corrective actions to previous events to prevent damage to a new fuel

assembly spacer grid strap during the final reload of the core in 2003. Following

discovery, the licensee entered the issue into its corrective action program. The primary

cause of this violation was related to the cross-cutting areas of corrective action and

human performance, because, despite earlier events, the licensee failed to adequately

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address the human performance issues that contributed to this and other fuel spacer

grid events.

Description: The licensee designated CR 02-06178 as a SCAQ CR. This CR described

repetitive damage to fuel assembly grid straps and rolled in the following CRs:

02-05645, 02-05895, 02-05896, 02-06343, and 02-09829. A root cause report was

required for CR 02-06178 as part of a NQA stop work order on fuel movements.

REVIEW OF ROOT CAUSE REPORT: The licensee issued a root cause analysis in

January 2003 which determined the cause of the repetitive grid strap damage. At this

time, the licensees CAP did not require use of a formal root cause process; however, a

formal TAPROOT process was used. Also, in May 2002, the licensee had completed a

root cause of fuel damage identified earlier in the outage. In reviewing the

January 2003 root cause report, the team noted several deficiencies:

The discussion on what occurred appeared to rely extensively on the previous

root cause, performed in May 2002, and on a 1999 Babcock and Wilcox (B&W)

root cause. The explanations for the statements made in the January 2003

report required understanding of the earlier studies in order to comprehend their

applicability.

The January 2003 root cause primarily focused on the new fuel assembly which

was discovered to be damaged in September 2002. It limited its discussion of

the other fuel assemblies discovered to be damaged in the September 2002 time

frame to listing the damage in a table and describing the disposition. This was

despite these CRs for these fuel assemblies being "rolled into" the root cause

report and a corrective action entry being closed with a statement that the root

cause report addressed the damage to the fuel assemblies.

The team noted that ten fuel assemblies were discovered to be damaged in

September through December 2002. This was in addition to the seven fuel

assemblies discovered to be damaged in March 2002. In one place in the

January 2003 root cause report, the licensee stated that the damage had to

occur during RFO 12, because there was no oxidation on fuel assemblies. The

team ascertained that, if the first statement was true, then the extent of condition

for the May 2002 root cause report must have been deficient in that it failed to

identify a number of damaged fuel assemblies.

In another section, the root cause report stated that review of the core loading

sequence determined that assembly NJ125Y, "and a number of other

assemblies," were loaded in a sequence that exposed those assemblies to

undesired corner to corner interactions. This second statement implied that the

damage might well have occurred during the fuel shuffle in March 2002.

However, the root cause report did not specifically identify which assemblies

were so loaded or otherwise follow up on this comment. The team determined

that a possible contributing cause was not identified or corrected.

The team noted that eight of the ten fuel assemblies discovered to be damaged

in September through December had only been burned once, and two were new

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fuel assemblies. Thus, the assemblies should not have been overly "bowed and

twisted," although this was listed as a possible reason for the damage.

In regard to the extent of condition, the team noted that the licensee provided an

extensive list of damage which occurred at other B&W sites. However, the only

Davis-Besse information from previous outages was from cycle 11. Data from

cycle 12 was missing from the table.

Based on the information in the extent of condition table, the team noted that,

approximately the same number of fuel assemblies were involved in both RFO

11 and 13. However, in RFO 11 the damaged fuel was mostly burned multiple

times and to have damage to only one or two grid strap locations. In RFO 13

(the current outage), the damaged fuel was primarily unburned or burned only

once and had damage to multiple grid strap locations.

The discussion on the December grid strap damage gave little credence to the

report that the fuel assembly was undamaged in September. Instead a

statement was made that because spacer grid 2 was damaged, and it hadn't

entered the pool, the damage must have occurred earlier. Given the extent of

the damage to the fuel assembly, the information provided in the CR initiation

statement from the personnel present, and the fact that only the northeast corner

face was damaged, the team considered it more likely that the damage occurred

all at one time.

The root cause report did not provide any discussion of the impact that occurred

during the December re-insertion. The team considered it unlikely that the

impact would not have caused any damage. The team noted that CR 02-09829

stated that the assembly visibly moved to the south. The team also noted that all

the damage occurred on the northeast corner. This indicated to the team that

the damage likely occurred during the re-insertion since a deflection to the south

would be an expected result if the northeast corner of the fuel assembly

impacted the cell. The failure to address why the impact occurred and the result

of the impact appeared to be a significant weakness in the root cause.

The team determined that no mention was made in the root cause report of

items such as whether the fuel handling personnel had the mast in fast or slow

speed or what the routine practice was regarding the fuel insertion rate.

Additionally, items such as length of time the crew had been working, schedule

pressures, and other factors which would address human performance were not

discussed, although these all could play a role in fuel handling mishaps.

FEBRUARY DAMAGE TO NEW FUEL ASSEMBLY: On February 24, 2003, during the final

reload of the cycle 14 core, another new fuel assembly was damaged. This was

documented in CR 03-01492. The licensee did an apparent cause evaluation for this

event and concluded that the damage to this fuel assembly was likely due to the less

than adequate design of the fuel assemblies. The team noted a number of issues that

did not appear to have been adequately considered in reaching the apparent cause

conclusion. For example:

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The damage occurred after the majority of the fuel assemblies were loaded and

only a few remained; this was not addressed in the apparent cause analysis.

The fuel handlers had spent approximately two hours unsuccessfully trying to

load another fuel assembly into place before deciding to change the loading

sequence to load another assembly in a potential corner to corner interaction

pattern. There was no indication that anyone suggested stopping the process

and evaluating the condition, before agreeing to the change in the loading

sequence.

Over the next three hours, multiple problems were experienced as the licensee

attempted to load the fuel assembly, including multiple overload conditions and

cable oscillations. The licensee reset the overload setpoints to the least limiting

condition at least twice, and even this setpoint was reached. Again, when

problems were encountered, the decision was to keep on trying to insert the

assembly, rather than stopping and evaluating what was happening.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to take adequate corrective actions in response to previous events and

as a result, a new fuel assembly spacer grid strap was damaged during the final reload

of the core in February 2003. Since there was a performance deficiency, the team

compared this performance deficiency to the minor questions contained in Appendix B,

"Issue Screening," of IMC 0612, "Power Reactor Inspection Reports." The team

concluded that the issue was more than minor because the licensee failed to prevent

recurrence of a significant condition adverse to quality as evidenced by damage to

previously undamaged fuel assembly grid straps. The team reviewed this finding in

accordance with IMC 0609, "Significance Determination Process. The barrier integrity

cornerstone was affected as failure of the grid straps has led to fuel leaks. No other

cornerstones were affected. There was one SDP Phase 1 worksheet question relating

to the fuel barrier. As this issue related to fuel barrier, the team concluded the issue

was of very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that

measures be established to ensure that conditions adverse to quality, such as

non-conformances, are promptly identified and corrected. For significant conditions

adverse to quality, it further requires that the cause is determined and corrective action

is taken to prevent recurrence.

Contrary to the above, as of February 5, 2003, the licensee had failed to take corrective

actions which prevented recurrence of grid strap damage, a significant condition

adverse to quality. Specifically on September 20, 2002, the licensee issued a stop work

order and a SCAQ was identified and documented in CR 02-06178. The root cause for

this report was completed in January 2003, prior to core reloading being allowed to

recommence. On February 5, a new fuel assembly was damaged after the licensee

made multiple unsuccessful attempts to insert the assembly into the core.

This issue was entered into the licensees CAP as CR 03-06996 at the end of the

inspection. Because this violation was of very low safety significance and because it

Enclosure

85

was entered into the licensees CAP, this violation is being treated as a NCV consistent

with Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-25).

(5)

Review of Fire Protection Corrective Action Items

a.

Inspection Scope

The team reviewed the licensees CAP to identify and address 10 CFR Part 50,

Appendix R, related deficiencies.

b.

Findings

.1

Process Monitoring Function for Alternative Shutdown Capability

Introduction: The team identified a Non-Cited violation of 10 CFR 50, Appendix R,

Section III.L.2.d having very low safety significance. Specifically, the issue regarded the

failure to provide necessary process monitoring readings for safe shutdown of the plant

during a fire event. The primary cause of this violation was related to the cross-cutting

area of problem identification and resolution because the licensee had previously

identified this issue as an enhancement and did not recognize that it was a violation of

regulatory requirements.

Description: During a review of the fire protection program, the licensee issued

CR 03-01648 identifying at failure to provide necessary process monitoring readings for

steam generator (SG) level and pressure necessary for safe shutdown of the plant

during a fire event. For the limiting Appendix R scenario (control room or cable

spreading room fire) where alternative shutdown was required, SG instrumentation

would not have been available for the idle SG during safe shutdown of the plant.

Without this SG level and pressure instrumentation, licensee operators would not have

been able to support the shell-tube differential temperature determination which was

required by the alternative shutdown procedure. This could have potentially resulted in

the loss of the thermal communication between the tubes and shell of the idle SG

resulting in unacceptable stresses on the tubes.

Even though the alternative shutdown procedures did not contain the necessary

procedural steps to prevent this condition if a fire in these areas were to occur,

operators could have taken temperature readings using a volt-meter to record the

temperatures locally at the penetration room. While these actions could not be credited

for the Appendix R analysis, they would be available. Additionally, after this

non-conformance was identified, the licensee performed a modification (ECR

03-0267-00) to provide level and pressure indication for the idle SG on the auxiliary

shutdown panel to support Appendix R safe shutdown.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to provide SG level and pressure indication required for alternative

shutdown. Since there was a performance deficiency, the team compared this

performance deficiency to the minor questions contained in Appendix B, "Issue

Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded

that the issue was more than minor because it affected the initiating events cornerstone

Enclosure

86

and, by not providing the direct indications necessary for the operators to determine the

status of the idle SG, the probability of experiencing unacceptable stresses on the SG

tubes during the limiting Appendix R scenario was increased.

The team reviewed this finding in accordance with IMC 0609, "Significance

Determination Process. The team determined this finding to be of very low

significance, based upon the low probability of a serious control room fire combined with

the low probability that such a fire would affect this specific instrumentation

detrimentally. Additionally, even in the event that such a fire had affected this

instrumentation, it was likely that the operators still would have been able to prevent

these tube stresses through use of manual actions, although this was not a credited

action in the Fire Protection procedures for this scenario. The team concluded the issue

was of very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix R, Section III.L.2.d states, in part, that the

process monitoring function for the alternative shutdown capability shall be capable of

providing direct readings of the process variables necessary to perform and control the

alternative shutdown.

Contrary to the above, the licensee did not provide SG level and pressure indication that

was required for the alternative shutdown scenario for the control room or cable

spreading room fire. The licensee entered the issue into its CAP as CR 03-01648.

Because this violation was of very low safety significance and because it was entered

into the licensees CAP, the violation is being treated as a NCV, consistent with

Section VI.A of the NRC Enforcement Policy. (NCV 05000346/2003010-26)

.2

Supporting Functions for Alternative Shutdown Capability

Introduction: The team identified a Non-Cited violation of 10 CFR Part 50, Appendix R,

Section III.L.2.e having very low safety significance. Specifically, the licensee failed to

provide the process cooling and lubrication necessary to permit the operation of the

equipment used for safe shutdown functions. The licensee entered the issue into its

corrective action program and performed a modification to resolve the issue. The

primary cause of this violation was related to the cross-cutting area of problem

identification and resolution because the licensee had previously identified this issue as

an enhancement and did not recognize that it was a violation of regulatory requirements.

Description: During a control room fire scenario, the governing procedure,

DB-OP-02519, Serious Control Room Fire, could not have been performed as written.

During this scenario, the procedure directed the operator to restore containment cooling

by resetting the #1 and #3 CACs. However, because of a modification to the control

circuitry of these CACs, the reset button on the outside of the CAC switchgear cabinet

was rendered non-functional.

Since the CACs were needed to ensure an acceptable containment atmosphere, without

them the potential existed that Appendix R credited equipment might not be functional

during a control room fire scenario due to heightened temperatures in the containment.

However, since the heatup in the containment was not instantaneous and since the

equipment would have to be subject to the heightened temperatures for a relatively long

Enclosure

87

period of time, the team considered it unlikely that the plant would have progressed to

an unrecoverable condition prior to the operators being able to recover containment

cooling. The licensee implemented a modification (ECR 03-0243-00) that rewired the

control circuitry for CAC fan 1-1 such that, in the case of a control room fire, this fan

could be started in slow speed to provide cooling to the containment.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to provide containment air cooling for alternative shutdown. Since there

was a performance deficiency, the team compared this performance deficiency to the

minor questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power

Reactor Inspection Reports." The team concluded that the issue was more than minor

because, if left uncorrected, the finding would become a more significant safety

concern. By not providing containment air cooling as per the governing alternative

shutdown procedure, the probability of the failure of equipment relied upon for safe

shutdown was increased. The team reviewed this finding in accordance with IMC 0609,

"Significance Determination Process. The team assessed the finding through Phase 1

of the reactor safety mitigating systems SDP. This issue was screened to be of very low

safety significance (Green) because there was not a total loss of safety function for an

assumed control room fire with evacuation. This was evaluated using the transient

without the secondary steam plant (TPCS) Phase 2 worksheet. Within the Phase 2

TPCS worksheet, the CAC supports the feed and bleed operation of the power operated

relief valve (PORV) for decay heat removal if the SGs are not available. Given this fire

scenario, the PORV block valve would be closed by procedure and the PORV not used,

so there was no effect on a safety function.

Enforcement: Title 10 CFR Part 50, Appendix R, Section III.L.2.e, states, in part, that

supporting functions shall be capable of providing the process cooling, lubrication, etc.,

necessary to permit the operation of the equipment used for alternative safe shutdown

functions.

Contrary to the above, the licensee did not adequately provide containment air cooling,

because the governing procedure did not reflect a recent modification that disabled the

Appendix R reset buttons for the #1 and #3 CACs. The CACs were required to support

operation of Appendix R equipment credited equipment. The licensee entered the issue

into its CAP as CR 03-02699 and 03-04341. Because this violation was of very low

safety significance and because it was entered into the licensees CAP, the violation is

being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy.

(NCV 05000346/2003010-27)

.3

Emergency Diesel Generator Floor Drains Design Deficiency

Introduction: The team identified a NCV of 10 CFR Part 50.48(a)(1), having very low

safety significance (Green). Specifically, the licensee failed to evaluate the adequacy of

EDG common floor drains following sprinkler system actuation in the fire affected EDG

room. Following discovery, the licensee entered the issue into its corrective action

process and revised the fire response procedures to address the issue.

Description: The team determined that the floor drains between the two EDG rooms

were common, and that they had insufficient drainage capacity. Preliminary calculations

Enclosure

88

by the licensee showed that the drains had a maximum capacity of 100 gpm, whereas

the sprinkler system actuation resulted in 303 gpm in Room 318, and 286 gpm in

Room 319.

Terminal blocks in both EDG control cabinets were located approximately seven inches

above floor level. The common drain lines between the EDG rooms would have allowed

suppression system water from a fire in one EDG room to enter and affect the integrity

of the redundant EDG room. As a consequence of a fire in one EDG room with

sprinkler system actuation, water would have backed up in both EDG rooms and would

have increased above the elevation of the terminal blocks within approximately 30

minutes. Furthermore, no operator or fire brigade instructions were in place to facilitate

drainage by opening of the doors to prevent equipment submergence. The licensee

initiated CRs 03-02577, 03-06901, and 03-07256 to document, evaluate, and disposition

these deficiencies in their CAP. As part of the corrective action, the licensee revised

pre-fire plans AB-318 and AB-319 to provide compensatory measures to prevent

flooding of the EDG rooms.

Analysis: The team determined that a performance deficiency existed because the

licensee failed to evaluate the adequacy of EDG common floor drains following sprinkler

system actuation. Since there was a performance deficiency, the team compared this

performance deficiency to the minor questions contained in Appendix B, "Issue

Screening," of IMC 0612, "Power Reactor Inspection Reports." The team concluded

that the issue was more than minor because the finding affected the mitigating system

cornerstone. This was a design deficiency that was confirmed not to result in the loss of

function per Generic Letter 91-18, Revision 1. The team reviewed this finding in

accordance with IMC 0609, "Significance Determination Process, and determined that

the issue was of very low safety significance (Green).

Enforcement: Title 10 CFR 50.48(a)(1) requires, in part, that each operating nuclear

power plant have a fire protection plan that satisfies Criterion III of 10 CFR Part 50,

Appendix A. Criterion III, requires, in part, that fire-fighting systems shall be designed to

assure that their rupture or inadvertent operation does not significantly impair the safety

capability of these structures, systems, and components.

Contrary to the above, because the EDG common floor drains were not evaluated by the

licensee, nor verified for adequacy following sprinkler system actuation, the potential

existed for an inadvertent sprinkler system actuation or rupture to adversely affect the

capability of the EDGs to perform their safety function. The licensee entered this issue

into its CAP as CRs 03-02577, 03-06901, and 03-07256. Because this violation was of

very low safety significance and because it was entered into the licensees CAP, the

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy. (NCV 05000346/2003010-28)

(6)

Review of Licensee Event Reports

a.

Inspection Scope

The team reviewed the licensees CAP to identify and address problems previously

identified and documented in licensee event reports.

Enclosure

89

b.

Findings

.1

(Discussed) LER 05000346/2002-008-00 and -01: Containment Air Coolers

Collective Significance of Degraded Conditions

Introduction: The team reviewed this LER which related to the operability of the CACs

during previous operating cycles.

Description: Following unit shutdown in 2002, various degraded conditions were

identified associated with the CACs, which were documented in several CRs. The

issues were related to thermal performance degradation, and structural issues

(CR 02-05563) related to seismic adequacy, boric acid corrosion, and post accident

thermal stress. Thermal performance issues caused by cooling coil fouling conditions

on the air (cooling fin) side, and water (inside tube) side were identified. Additionally,

foreign material (plywood) was found in the SW supply piping to CAC # 2. In addition,

two 10 CFR Part 21 reports were issued by the CAC control vendor and the motor

vendor. The overall corrective action to resolve the physical degradation of the CAC

units was the refurbishment of the units prior to plant restart. New CAC units were

installed.

An engineering evaluation was performed to assess the effects of the degraded

conditions on heat transfer capability from which past operability was determined. The

licensee concluded that the effects of the degraded conditions (including foreign

material in the cooling water line) on heat transfer capability of the CACs, when

operating in conjunction with the CS system, would not have rendered the CACs

inoperable with respect to the long term post-accident containment heat removal

capability. These evaluations included containment pressure reduction, increased sump

temperature effects on ECCS pumps NPSH, ECCS pump room heatup, equipment

environmental qualification, and radiological release. A NCV was identified in Section

4OA3(3)b.3, for failure to implement effective design control measures to check and

verify the adequacy of the design basis calculation performed for offsite dose

consequences of degraded CACs.

The licensee performed an engineering evaluation of the structural issues and

concluded that the issues resulted in a degraded condition, but the CACs were not

rendered inoperable. The licensee stated that, while corrosion and pitting were

observed, the "as found" condition would not have been sufficiently degraded to prevent

the CACs from performing as seismically designed.

The licensee determined that the station had no safety related parts applicable to the

10 CFR Part 21 notification made by the controls vendor. At the time of receipt of the

Part 21 notification from the motor vendor, the licensee stated that the plant was in

Mode 6 and the CAC motors were being refurbished as part of the overall CAC

refurbishment. The notification reported a deficiency with a stator winding, which could

result in motor winding failure. According to the licensee, no winding failures or

anomalies were experienced during fan operation.

During review of the LER, the team identified several concerns with the licensees

evaluation. For example:

Enclosure

90

The licensee stated in the LER that "Since the service conditions for CACs #1

and #2 are similar to CAC #3, the degraded conditions on CAC #3 were

considered to be representative of the other CAC cooling coils." However, the

team determined that the #3 CAC was normally in standby, with CACs 1 and 2

being in operation. Therefore, the team could not agree that the condition in

CAC 3 was representative of the condition of the other two CACs.

The licensee noted that "a piece of plywood measuring approximately 5 inches

by 7 inches was discovered in the 8-inch diameter supply line upstream of the

transition to two 6-inch pipes, each of which supplies SW to one of two

independent cooling coil manifolds." The licensee stated that the presence of

the plywood was believed to be an isolated condition that occurred during RFO

12 in 2000. However, the licensee did not provide any information as to work

performed during RFO 12 which would have resulted in leaving a piece of

plywood behind. The licensee also noted that there were no intervening pipe

fittings or valves between the as-found location of the foreign material and the

two 6-inch transitions; however, the licensee did not provide any further

justification why the SW flow to this CAC would not be disrupted during a design

basis event.

In the thermal performance analysis section the licensee stated that, "Air side

degradation consisted of boric acid residue and dirt which may impede the heat

transfer characteristic of the cooling fins." However, in the preceding section on

structural issues, the air side was characterized as having "moderate to severe

corrosion" and noted that "corrosion and pitting" were observed. The licensee

did not explain why the two sections differed, much less explain difference in

heat transfer characteristic impact from "residue and dirt" to that obtained from

"corrosion and pitting."

The LER also stated that, "operation of the CAC units was directly into high fan

speed for normal operation." This statement did not address the fact that during

response to an accident, the two operating fans would shift from high to low

speed. Shifting from high to low speed was one of the factors mentioned in the

Part 21 report on the motors as causing motor failures. It also did not mention

that the motor on the normally operating CAC 1 was replaced during a mid-cycle

outage in 1999.

The licensee's conclusion that the effects of the degraded conditions on the heat

transfer capability of the CACs, when operating in conjunction with the CS

system did not address the fact that the CS system was also degraded due to

the previously identified sump issues.

During the review of this LER, the team identified additional issues concerning the

original motor sizing calculation and the lack of thermal relief valves on the CAC SW

piping inside containment as described in Sections 4OA3(3)b.3. Because of the overall

deficiencies in the licensee's evaluation, especially in regard to the thermal performance

issue, the team was unable to agree with the licensee's conclusion that the CACs were

operable during previous cycles.

Enclosure

91

The team determined that this LER will remain open pending further review of the CAC

degradation; specifically the extent of degradation and effect on the safety function of

the CACs. For this particular LER, the additional reviews will provide information as to

the ability of the CACs to provide cooling for the PORVs during feed and bleed

operations. The LER will remain open pending resolution of this issue.

.2

(Closed) LER 05000346/2002-009-00: Degradation of the High Pressure

Injection Thermal Sleeves

On November 29, 2002, with the reactor defueled, it was discovered that the thermal

sleeve connected to the 2-2 HPI /makeup nozzle had an axial crack. Inspection of the

2-1 HPI/makeup thermal sleeve also revealed a cracked thermal sleeve. No cracking

was observed during the inspection of the remaining two HPI thermal sleeves. The

licensee reported that the nozzles with undamaged thermal sleeves had not been used

for RCS makeup. The licensee determined that the axial cracks identified in the thermal

sleeves did not affect the ability of the HPI system to perform its design function nor did

either crack provide a source for RCS pressure boundary leakage. Furthermore, since

no loss of material occurred, this condition had no impact on the integrity of the fuel

cladding.

Upon discovery of the cracks in both thermal sleeves, the sleeves were removed and

new ones were installed. The licensee determined that high cycle thermal fatigue was

the root cause of the identified cracking. A contributing cause was the rate and

oscillation of makeup flow through the primary makeup nozzle. The licensee stated that

the appearance of the cracked sleeves was consistent with cases observed at other

B&W plants.

The remedial action was to replace the thermal sleeves. Inservice inspection

procedures were developed to ensure proper inspection techniques were used in the

future to verify the integrity of the HPI/makeup thermal sleeves. The licensee stated

that the visual inspections will include the use of high resolution video equipment and

verification that the video equipment was applied in accordance with ASME Section XI,

sub-article IWA 2210, Visual Exam for VT-1 Examination. The licensee stated that the

frequency of inspection would be every other refueling outage. This issue was entered

into the licensees CAP as CRs 02-09739, 02-9928, and 03-02445.

The team reviewed the licensee's corrective actions and determined them to be

acceptable. No violation of regulatory requirements was identified. This item is closed.

.3

(Closed) LER 05000346/2003-003-00 and -01: Potential Inadequate High

Pressure Injection Pump Minimum Recirculation Flow Following a Small Break

Loss of Coolant Accident

Introduction: The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

having very low safety significance (Green). Specifically, the licensee failed to provide

for the original plant design to incorporate a safety-related recirculation path for the HPI

pumps in the HPR mode of operation. Following discovery, the licensee entered the

issue into its corrective action process.

Enclosure

92

Description: Following the questioning during the 2002 NRC SSDI inspection of a

potential deadhead condition of the HPI pumps and the adequacy of thermal protection

(minimum flow) for the pumps, the licensee performed a study, 86-5022260-00, to

determine whether HPI pump operability during post-LOCA sump recirculation could be

assured for all break sizes and transient scenarios.

This study identified a range of small break sizes from 0.00206 ft2 (leak-to-LOCA

transition area) to 0.0045 ft2, which would result in RCS re-pressurization cycles that

could continue following HPI pump realignment to the containment emergency sump

and closure of the minimum flow recirculation valves. The study concluded that for this

newly analyzed range of break sizes, past operability of the HPI pumps was a concern.

This was because the re-pressurization cycles would result in a higher RCS pressure

than the shut-off head of the HPI pumps, resulting in pump dead heading (no flow),

when HPI pump suction was from the sump. The licensee documented this condition in

CR 02-06702 and LER 05000346/2003-003. The condition existed since the original

design of Davis-Besse. The NRC had previously highlighted the potential for this

concern as part of Information Notice (IN) 85-94.

Based on the results of the evaluation, several corrective actions were implemented. An

additional minimum flow recirculation line was installed during RFO 13 for each HPI

pump. For one pump, the line tapped off the previously existing minimum flow line and

for the other a completely new recirculation line was installed. For both pumps, the new

lines contained two isolation valves and a non-cavitating pressure breakdown orifice and

connected to the low pressure injection (LPI) pump discharge upstream of its respective

decay heat cooler for the corresponding safety train. These additional recirculation lines

were designed to provide the original minimum flow protection of the HPI pumps,

35 gpm, when aligned to the emergency sump in "piggyback" operation with the DHR

pumps. In this lineup, the decay heat coolers would provide cooling for the respective

HPI Pumps without loss of sump inventory.

Operator action would be required to open the valves on these additional recirculation

lines prior to pump realignment from the BWST to the emergency sump. Because the

postulated transient was a very slow developing scenario, the team determined that

ample time would be available for operators to take this action. Additionally, the team

confirmed that this action did not replace any existing automatic action. The licensee

revised the emergency procedures to provide direction on establishing the HPI alternate

minimum recirculation flowpath and provided training to the operators on its use.

These corrective actions were deemed to be sufficient to resolve the concern addressed

in the LER. See Section 4OA3(3)b.1, for further discussion regarding the adequacy of

the 35 gpm minimum recirculation flow.

Analysis: The team determined that a performance deficiency existed because the

original design did not incorporate a safety-related recirculation path for the HPI pumps

in the high pressure recirculation (HPR) mode of operation. Since there was a

performance deficiency, the team compared this performance deficiency to the minor

questions contained in Appendix B, "Issue Screening," of IMC 0612, "Power Reactor

Inspection Reports." The team concluded that the issue was more than minor because

the licensee failed to provide for the original plant design to incorporate a safety-related

Enclosure

93

recirculation path for the HPI pumps in the HPR mode of operation and this finding

affected the mitigating systems cornerstone. The team reviewed this finding in

accordance with IMC 0609, "Significance Determination Process.

The Region III SRAs, evaluated this issue within Phase 1 of the SDP. Based on the

review, the SRAs determined that the HPR safety-function would not actually have been

lost because of reliance on procedure actions for feed and bleed operation of the PORV

in situations where the SGs could not be used to remove decay heat. Specifically, for

initiating events where RCS leakage was not sufficient to remove decay heat

(transients, small LOCAs) the Phase 2 SDP plant specific notebook for Davis-Besse

takes credit for opening of the non-safety-related PORV to remove decay heat from the

RCS. Opening of the PORV would allow sufficient HPR flow to ensure adequate

minimum flow to ensure pump cooling. Therefore, the finding screened out as having

very low safety significance (Green).

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, requires, in part, that

measures be established to assure that applicable regulatory requirements and the

design basis were correctly translated into specifications, drawings, procedures, and

instructions. Furthermore, it requires that measures be provided for verifying or

checking the adequacy of design, such as by the performance of design reviews, by the

use of alternate or simplified calculational methods, or by the performance of a suitable

testing program.

Contrary to the above, the licensee failed to provide for the original plant design to

incorporate a safety-related recirculation path for the HPI pumps in the HPR mode of

operation. The licensee documented this condition in CR 02-06702. These corrective

actions were deemed to be sufficient to resolve the concern addressed in the LER.

Since the issue was of very low safety significance and was captured in the licensee's

CR, it is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement

Policy. (NCV 05000346/2003010-29)

4OA4 Cross-Cutting Aspects of Findings

The teams findings and observations, as documented in this report, revealed numerous

examples where the licensees corrective action program exhibited implementation

weaknesses and a general lack of engineering rigor in the conduct of engineering

activities. These concerns further represent deficiencies relating to the cross-cutting

areas of human performance and corrective actions. Specific deficiencies and concerns

supporting this conclusion are documented in sections listed below.

Findings Affecting Human Performance

4OA3(2)b.2

Lack of 480 Vac Class 1E Motor Thermal Overload Protection

4OA3(3)b.6

Non-conservative Calculation Used in Design Analysis to Determine

Required Service Water Makeup Flow to Component Cooling Water

4OA3(3)b.11 Service Water Discharge Path Swapover Setpoint

4OA3(3)b.12 Service Water Discharge Check Valve Test Acceptance Criteria

4OA3(3)b.14 Auxiliary Feedwater System Calculation Issues With Main Steam Safety

Valves

Enclosure

94

4OA3(3)b.21 Environmental Qualification of Equipment Not Supported by Analysis

4OA3(3)b.23 Inappropriate Application of 10 CFR 50.59

4OA3(4)b

Repetitive Spacer Grid Strap Damage

Findings Affecting Corrective Action Program

4OA3(2)b.3

Failure to Perform Adequate Direct Current Contactor Testing to Ensure

Minimum Voltage at Motor Operated Valves

4OA3(2)b.4

Failure to Verify Adequacy of Short Circuit Protection for Direct

Current Circuits

4OA3(2)b.5

Lack of Calculations to Ensure Minimum Voltage Availability at

Device Terminals

4OA3(3)b.1

High Pressure Injection Pump Operation Under Long Term Minimum

Flow

4OA3(3)b.2

Increased Dose Consequences Due to Degraded Thermal Performance

Operation of Degraded Containment Air Coolers

4OA3(3)b.3

Containment Air Cooler Air Flow Calculation Concerns

4OA3(3)b.7

Calculation Concerns for Service Water Pump Room Ventilation System

4OA3(3)b.11 Service Water Discharge Path Swapover Setpoint

4OA3(3)b.12 Service Water Discharge Check Valve Test Acceptance Criteria

4OA3(3)b.13 Lack of Design Basis Calculations to Support Service Water Single

Failure Assumptions

4OA3(3)b.15 Auxiliary Feedwater Strainer Mesh Size and Preconditioning of Auxiliary

Feedwater System During Testing

4OA3(3)b.19 Inadequate Evaluation of Reactor Coolant Pump Casing-to-cover Stud

Overstressing

4OA3(4)b

Repetitive Spacer Grid Strap Damage

4OA3.(5)b.1

Process Monitoring Function for Alternative Shutdown Capability

4OA3.(5)b.2

Supporting Functions for Alternative Shutdown Capability

4OA5 Other Activities

(1)

Assessment of the Licensees Corrective Actions to Address Previously Identified

Findings Documented in NRC Reports

a.

Inspection Scope

The team conducted a review of previously identified items to determine effectiveness of

identification, evaluation and resolution of issues.

b.

Findings

.1

Follow up on Findings Documented in Report 05000346/2002012

.1

(Closed) URI 05000346/2002012-02: Potential Impact of Corrosion on the

Ground Function of Electrical Conduit in Containment

During a previous inspection conducted in October 2002, the NRC team noted that

corrosion appeared to be particularly concentrated in areas where moisture and boric

Enclosure

95

acid from the containment atmosphere had condensed and dripped onto electrical

components. In particular, the NRC team noted substantial corrosion and deposits of

crystallized boric acid on conduits. Based on this observation, the NRC team identified

a concern that boric acid corrosion of conduit may create a high electrical resistence

and challenge the ground function of the electrical conduit.

This condition was documented by the licensee in CR 02-06788. The CR described a

condition where boric acid corrosion of conduits in the containment could inhibit the flow

of ground fault currents through the conduits (conduits provide a supplementary

grounding path for smaller motors).

The cause analysis for CR 02-06788 determined that, as a general rule, up to 50

percent loss of conduit cross sectional area was acceptable without loss of function as

an electrical ground path. The conduits in question were determined to have only

surface corrosion amounting to less than 25 percent reduction in cross sectional area

and were therefore, deemed acceptable.

Subsequently, CR 03-05239 was issued stating that no loss in wall thickness was

acceptable for1/2-inch and 3/4-inch conduits. Ultrasonic testing was performed to

determine the wall thickness of corroded conduits; however, no decision had been made

as to resolution of this issue. Following questions by the team, the licensee determined

that all conduits were acceptable as-is. Based on this conclusion, the team determined

that no violation of NRC requirements existed. This URI is considered closed.

.2

(Closed) URI 05000346/2002012-03: Potential Failure to Follow the Procedure

for Raychem' Splice Removal on Electrical Cables

During CAC motor replacement, the licensee identified splitting of the motor cable

insulation as documented in CR 02-05459. The resolution of this issue is discussed in

Section 4OA3(2)b.6. The URI is closed.

.2

Follow-up on SSDI Findings Documented in Report 05000346/2002014

.1

(Discussed) NCV 05000346/2002014-01a: Lack of a Design Basis Analysis for

Containment Isolation Valve Backup Air Supplies

This violation was written to document an issue regarding the CAC outlet SW valves

reliance on the availability of the non-seismic instrument air system to maintain pressure

on the air operated valves so that they could perform their containment isolation function

to remain closed. The resolution of this issue is discussed in Section 4OA3(3)b.4.

.2

(Discussed) NCV 05000346/2002014-01b: Inadequate Blowdown Provisions for

Containment Air Cooler Backup Air Accumulators

This violation was written to document that there was no provisions to blow down the

CACs to remove excessive moisture as required by the USAR. The acceptability of the

corrective actions to this issue is discussed in Section 4OA3(3)b.5.

Enclosure

96

.3

(Closed) URI 05000346/2002014-01c: Failure to Perform Comprehensive

Moderate Energy Line Break Analysis

This item dealt with the licensees failure to perform a comprehensive moderate energy

line break analysis. The resolution of this issue is discussed in Section 4OA3(3)b.24.

The URI is closed.

.4

(Closed) URI 05000346/2002014-01d: Lifting of Service Water Relief Valves

This URI dealt with a continuing operating condition when the relief valves on the tube

(SW) side of the CCW heat exchangers would open when the licensee changed which

pump was operating under low flow conditions such as winter operation with low heat

loads. The licensee resolved the problem of inadvertent openings by changing the

operating procedures. The team concluded that relief valve lifting was not a concern

during a design basis event because there would be an increased heat load. This would

prevent the underlying pressure surge from occurring. No violation of NRC

requirements was identified. This item is closed.

.5

(Closed) URI 05000346/2002014-01e: Inadequate Service Water Pump Room

Temperature Analysis

This URI concerned non-conservatisms in the analysis which analyzed the heat loads in

the SW pump room and the ability of the ventilation system to maintain the pump room

temperatures within a required operating range. The resolution of this issue is

discussed in Section 4OA3(3)b.7. The URI is closed.

.6

(Closed) URI 05000346/2002014-01f: Inadequate Service Water Pump Room

Steam Line Break Analysis

This item dealt with the effects of a postulated auxiliary steam line break in the SW

pump room and whether the licensee correctly translated the USAR commitments

regarding the SW pump room environmental limits into analyses that demonstrated

these limits would not be violated for design basis conditions. This issue is discussed in

Section 4OA3(3)b.7. The URI is closed.

.7

(Closed) URI 05000346/2002014-01g: Inadequate Cable Ampacity Analysis

On September 24, 2002, the licensee issued CR 02-06893 to document an increase

from 95F to 124F in Rooms 105 and 115 temperature as a result of an increase of

SW temperature. The CR identified the need to reevaluate cable ampacity as a result of

the higher room temperature. The team discussed the ampacity issue with the licensee,

and determined there actually was not an ampacity concern. Therefore, this item is

considered closed.

Enclosure

97

.8

(Closed) URI 05000346/2002014-01h: Inadequate Flooding Protection for

Service Water Pump House

This URI dealt with deficiencies in correctly implementing USAR commitments regarding

flood protection for the SW pump room. The resolution of this issue is discussed in

Section 4OA3(3)b.9. The URI is closed.

.9

(Discussed) NCV 05000346/2002014-01i: Non-conservative Technical

Specification Value for 90 Percent Undervoltage Relays

The licensee initiated CR 02-07766 to address the issue that the trip set point specified

in calculation C-EE-004.01-049 was greater than the TS allowable value shown in Table

3.3-4. Therefore, the postulated TS allowable value could be violated for plant operating

conditions where the voltage was just above the relay set point value. The team

reviewed the issue and determined that the new calculation, C-EE-015.03-008, which

utilized the ETAP program, properly addressed all issues included in the CR. Therefore,

the corrective actions to this issue were deemed acceptable. Another issue related to

allowable values is discussed in Section 4OA3(2)b.1.

.10 (Closed) URI 05000346/2002014-01j: Poor Quality Calculation for 90 Percent

Undervoltage Relays

The licensee entered the issue into its CAP as CR 02-07633 which subsequently was

rolled over to CR 02-07646. In order to resolve the concern, the licensee performed a

new calculation, C-EE-015.03-008, to address this and other electrical issues. Review

of the calculation is discussed in Sections 4OA3(2)b.7 and 4OA5(1)b.2.11. This item is

closed.

.11 (Discussed) NCV 05000346/2002014-01k: Non-conservative Relay Setpoint

Calculation for the 59 Percent Undervoltage Relays

The licensee initiated CR 02-06737 and CR 02-07646 to evaluate issues affecting the

relay uncertainty in calculation C-EE-004.01.051. The postulated inconsistencies could

have rendered the operation of the 59 percent relay inconsistent with requirements for

continuous operation under-voltage transient conditions imposed by the motor inrush

current.

The team reviewed CR 02-07646 and determined that calculation C-EE-015.03-008,

which used the ETAP program described in Section 4OA3(2)b.7, had properly

addressed the postulated inconsistencies and non-conservative assumptions in the

uncertainty analysis. Therefore, the corrective actions to this issue were deemed

acceptable.

Enclosure

98

.12 (Closed) URI 05000346/2002014-01l: Inadequate Calculations for Control Room

Operator Dose (GDC-19) and Offsite Dose (10 CFR Part 100) Related to High

Pressure Injection Pump Minimum Flow Values

This URI addressed concerns with the dose calculations for operators and the general

public following a design basis accident. The resolution of this issue is discussed in

Section 4OA3(3)b.18. The URI is closed.

.13 (Closed) URI 05000346/2002014-01m: Other GDC-19 and 10 CFR Part 100

Issues

This URI addressed concerns with the dose calculations for operators and the general

public following a design basis accident. The resolution of this issue is discussed in

Section 4OA3(3)b.18. The URI is closed.

.14 (Closed) URI 05000346/2002014-01n: High Pressure Injection Pump Operation

Under Long Term Minimum Flow

This item dealt with the ability of the HPI pumps to perform as intended during extended

operation on minimum flow. This issue is discussed in Sections 4OA3(3)b.1 and

4OA3(6)b.2. This URI is closed.

.15 (Closed) URI 05000346/2002014-01o: Some Small Break Loss of Coolant

Accident Sizes Not Analyzed

This URI addressed concerns with the HPI pump potentially not having a flow path upon

the suction being switched from the BWST to the sump. This issue is discussed in

Section 4OA3(6)b.3. This URI is closed.

.16 (Closed) URI 05000346/2002014-01p: Inadequate Service Water System Flow

Analyses

This URI dealt with deficiencies in the assumptions used in SW system flow

calculations. The resolution of this issue is discussed in Section 4OA3(3)b.8. The URI

is closed.

.17 (Closed) URI 05000346/2002014-01q: Inadequate Service Water System

Thermal Analyses

This URI dealt with deficiencies in the maximum temperatures used in SW system and

ultimate heat sink calculations. The resolution of this issue is discussed in Sections

4OA3(3)b.8 and 4OA3(3)b.13. The URI is closed.

.18 (Closed) URI 05000346/2002014-01r: Inadequate Ultimate Heat Sink Inventory

Analysis

This URI dealt with deficiencies in the SW system flow and ultimate heat sink minimum

level calculations. The resolution of this issue is discussed in Sections 4OA3(3)b.8 and

4OA3(3)b.13. The URI is closed.

Enclosure

99

.19 (Closed) URI 05000346/2002014-01s: No Valid Service Water Pump Net

Positive Suction Head Analysis

This URI dealt with the licensee not having a calculation which showed that the SW

pumps had adequate NPSH under all operating conditions. The resolution of this issue

is discussed in Section 4OA3(3)b.8. The URI is closed.

.20 (Closed) URI 05000346/2002014-01t: Service Water Source Temperature

Analysis for Auxiliary Feedwater

This item dealt with SW source for AFW which had not been analyzed with respect to its

potentially higher temperature condition for various design basis events and the possible

impact on the ability of the AFW system to perform its safety function. Such effects

could include reduced heat absorption capability for AFW injected into the SGs and

inadequate cooling of AFW lubricating oil. The licensees evaluation concluded that

temperature of AFW (seismic event with long term AFW supplied by SW) was lower

than the design AFW temperature of 120F as noted in the system description. In

addition, the licensee determined that AFW equipment temperature limits were greater

than 120F. Therefore, the licensee concluded that there was no discrepant condition.

The team agreed with this assessment. This URI is closed.

.21 (Closed) URI 05000346/2002014-01u: Inadequate Short Circuit Calculations

This URI was written to document that the licensee had not considered the worst case

grid voltage. The resolution of this issue is discussed in Section 4OA3(2)b.8. The URI

is closed.

.22 (Discussed) NCV 05000346/2002014-01v: No Analytical Basis for Setpoint to

Swap Service Water System Discharge Path

There was no analytical basis for the setpoint used to swap the SW system discharge

path from the normally used, but non-seismic lines, to a seismically qualified path. The

setpoint for the swapover was 50 psig; however, there was no calculational bases for

this setpoint. The acceptability of the corrective actions to this issue is discussed in

Section 4OA3(3)b.11.

.23 (Discussed) NCV 05000346/2002014-02a: Service Water Surveillance Test Did

Not Use Worst Case Values

This violation addressed the fact that a surveillance test did not demonstrate that

worst-case post-accident conditions were bounded for the CAC discharge valves in the

SW system.

The licensee was replacing these valves, due to a number of problems with them. The

proposed corrective actions appeared to include appropriate acceptance criteria. The

team identified a concern with the original evaluation and corrective action wording in

CR 02-07781. The NCV writeup mentioned that the licensees procedure did not

declare the valves inoperable and write a CR if the valves failed the valve closure test.

This issue was not originally addressed in the licensees corrective actions. However,

Enclosure

100

when it was brought to the licensees attention, appropriate changes were made in the

procedure to address declaring the valve inoperable and writing CRs when necessary.

In responding to a team request for supporting calculations, the licensee also noted that

a corrective action for the CR 02-07781 was closed prior to a calculation being reviewed

and approved. Other examples where corrective actions were closed prior to the

calculations being approved are discussed in Sections 4OA3(3)b.17 and 4OA3(3)b.19.

.24 (Closed) URI 05000346/2002014-02b: Inadequate Service Water Flow Balance

Testing

This URI was written to document concerns with the flow balance testing for the SW

system. The resolution of this issue is discussed in Section 4OA3(2)b.10. This URI is

closed.

.25 (Closed) URI 05000346/2002014-03a: Inappropriate Service Water Pump Curve

Allowable Degradation

In the 2002 NRC SSDI, the team identified an item associated with prompt corrective

action to resolve a the licensee identified condition where the allowable degradation of

the SW pumps did not match the design basis required flow rate for the SW pumps. In

particular, the pump curve was allowed to degrade by 7 percent in accordance with IST

acceptance criteria, without evaluating the required design basis flow requirement.

Vendor calculations02-123 and 02-113 were performed to address all SW hydraulic

issues. The allowable SW pump degradation was included in the new calculations. The

team did not identify any violation. This URI is closed.

.26 (Closed) URI 05000346/2002014-03b: Repetitive Failures of Service Water

Relief Valves

This URI, URI 02-14-01d, and URI 02-14-06 all dealt with a continuing operating

condition where the relief valves on the tube (SW) side of the CCW heat exchangers

were opening under routine operating conditions, were failing due to the frequent

opening, and to the licensee's stated plans to resolve the problem by removal of the

valves from the system, contrary to the requirements of the ASME Code.

At the time of the inspection, the licensee had not yet removed the relief valves;

therefore, the issues raised by the URI still existed. The licensee had taken a number of

actions to reduce the frequency of undesired relief valve openings, primarily through

changes in the operating procedures. The licensee stated that these procedural

changes greatly decreased the times that the valves opened unexpectedly. The

reduction in inadvertent openings also resulted in a reduction of valve failures.

The team considered The licensees plans to remove the relief valves to be

inappropriate as the team did not believe the ASME Code allowed for the valves to be

removed. The team reviewed the applicable sections of both ASME Section III (the

Code section applicable to the SW piping) and ASME Section VIII (the Code section

under which the heat exchangers were purchased). Both sections clearly indicated that

overpressure protection was required for any piping where heat was being introduced

into the system. As the SW system was the cooling mechanism for the CCW heat

Enclosure

101

exchangers, heat was being introduced into the system, and overpressure protection

was required. The team also noted that the licensee had manual valves downstream of

the relief valves on the CCW heat exchangers; another area which was not in strict

compliance with the Code. Subsequent to the inspection, the licensee informed the

team that a decision had not been made to replace the subject valves. Since the

licensee has not removed the valves from service, this URI is closed.

The issues regarding URI 50-345/2002014-06 will be addressed in a separate report.

.27 (Closed) URI 05000346/2002014-03c: Non-conservative Difference in Ultimate

Heat Sink Temperature Measurements

This URI dealt with a potential non-conservative temperature measurement for ultimate

heat sink temperatures. The concern was that the temperature instrument used to

measure the ultimate heat sink temperature might not be the most conservative and

might contain up to 2F of error, which was not accounted for in the SW design basis

calculations.

The licensee performed a test which measured the temperature of the ultimate heat sink

in two different locations - the normal input for the computer point, and a second one

which had been reading higher during the October inspection - using sensitive,

calibrated measuring and test equipment. Based on this test, the licensee determined

that the two locations were reading the same temperature, at least at the time of the

test. The licensee also noted that the normal temperature instrument had a much

tighter accuracy band (0.75F) as compared to the other instrument (3F) such that,

even if the second instrument appeared to be reading higher, it might actually be below

the actual ultimate heat sink temperature.

The team determined that the licensees procedures had been revised to incorporate the

temperature instruments uncertainty calculation results into them, and that the

procedures required the plant to take appropriate actions should it appear that the

ultimate heat sink temperature was being approached (such as measuring the

temperature locally with sensitive measuring and test equipment). Therefore, the team

determined that no violation existed. This URI is closed.

.28 (Discussed) NCV 05000346/2002014-03d: Inadequate Corrective Actions

Related to Service Water Pump Discharge Check Valve Acceptance Criteria

This violation addressed an inadequate corrective action in that the acceptance criterion

for the inservice full flow test for the SW pump discharge check valves was determined

to be non-conservative, was corrected, and the new value was still not the full design

flow rate. The acceptability of the corrective actions to this issue is discussed in Section

4OA3(2)b.12.

.29 (Closed) URI 05000346/2002014-03e: Non-conservative Containment Air

Cooler Mechanical Stress Analysis

This item dealt with overestimation of nozzle flexibility by a factor of one thousand when

analyzing the connection of the SW system to the CACs. This item was also briefly

discussed in the section for LER 05000346/2002-008-00 and -01.

Enclosure

102

Stress analyses concluded that the CACs were operable in the past regarding structural

concerns identified in CR 02-05563. The structural report concluded that, "...Based on

the lack of significance or the continued structural acceptability identified with the

numerous finding associated with the CAC coil modules and their support structure, the

CAC operability assessment is considered to be unaffected by the composite findings of

all currently identified, structural-related CAC concerns. The team determined that the

licensee appropriately used ASME Code F stress criteria in the structural analysis. This

item is closed.

.30 (Discussed) NCV 05000346/2002014-04: Failure to Perform Technical

Specification Surveillance for High Pressure Injection Pump Following

Maintenance

This item dealt with the failure to perform a surveillance in accordance with TS 4.5.2.H

for HPI pump following maintenance. This TS could not be directly verified by test since

system pressure could not be easily held at 400 pounds per square inch, absolute

during full HPI injection. The licensee requested a TS amendment (No. 256) to relocate

the surveillance requirement pertaining to flow balance testing of the HPI and LPI

subsystems following system modifications to the technical requirement manual. Also,

the amendment added ECCS pump operability conditions to the TS. The new

surveillance requirement would require verifying each ECCS pumps developed head to

be greater than or equal to the required developed head, when tested pursuant to TS

4.0.5 with regards to inservice testing requirements of the ASME Code. The team had

no further concerns and did not identify other new issues.

.31 (Closed) URI 05000346/2002014-05: Question Regarding Definition of a

Passive Failure

This URI dealt with the question on whether stem-to-disc separation of SW valve SW-82

was credible and whether stem-to-disc separation was required to be assumed as part

of a passive failure analysis. The team determined that valve SW82 was a butterfly

valve. Even if stem-to-disc separation occurred, it was extremely unlikely that flow

would be blocked. Therefore, the team determined that this failure mode was not

credible and did not need to be considered as part of a passive failure analysis. As

discussed in Sections 4OA3(3)b.11 and 4OA3(3)b.13, the team identified other

concerns with the licensee's consideration of passive failure assumptions; these

concerns are addressed separately. This URI is closed.

.3

Follow-up on SSDI Findings Documented in Report 05000346/2002019

(Closed) URI 05000346/2002019-031: Final Evaluation of Apparent Cause

Evaluation for LER 05000346/2002-006-00

This URI was opened to track the licensee's resolution of the issues identified in LER

05000346/2002-006 on EDG exhaust stack tornado protection. This issue is discussed

in Section 4OA3(3)b.23, of this report. This URI is closed.

Enclosure

103

.4

Follow up on Augmented Inspection Team Findings Documented in the Cover

Letter of Report 05000346/2003016

In the cover letter of IR 05000346/2003016, a number of URIs identified in IR

05000346/2002008 were converted from URIs to apparent violations (AVs). The

numbering of the individual items remained the same. The team reviewed the status of

each of the AVs, as documented below.

.1

(Discussed) AV 05000346/2003016-01: Technical Specification Reactor Coolant

System Pressure Boundary Leakage

Introduction: The NRC team examined corrective actions for an AV of the Davis-Besse

TS associated with operation of the plant with pressure boundary leakage from

through-wall cracks in the RCS.

Description: The team determined that this AV was a product of the licensees cultural

and programmatic breakdowns. Operation with pressure boundary leakage beyond the

TS action statement was a direct result of the licensees failure to identify the control rod

drive mechanism leakage. The cultural issues involved the failure to take appropriate

corrective actions, to follow procedures, and to have appropriate procedures; issues that

were identified in the subsequent findings of the AIT follow-up report. The specific

programmatic issues were identified in LER 05000346/2002-002-00 as an inadequate

BACC program and inadequate implementation of the ISI program.

Corrective actions for the cultural failures were addressed by globally by the licensees

management and human performance improvement plan and the program compliance

plan. Corrective actions for the failure to take appropriate action were specified under

CR 02-00891 and directed a complete overhaul and re-institution of the CAP. The

NRCs assessment of the effectiveness of those actions is discussed in Sections 4OA2

and 4OA3 of this report.

Corrective action for the inadequate BACC program is discussed below in Section

4OA5(1)b.4.8. Inadequate implementation of the ISI program was addressed through

licensee self-assessment 2002-081 and a Phase 2 program review by the project review

committee (PRC).

Analysis: This issue represented a licensee performance deficiency because the

licensee had multiple opportunities over a period of years to identify the leakage;

consequently it was considered a finding. This finding was of more than minor safety

significance because the RCPB and resultant cavity in the reactor vessel head

represented a loss of the design basis barrier integrity. Two cornerstones were

impacted by this issue. The barrier integrity cornerstone was affected because the

through-wall CRDM cracks compromised the RCPB and the initiating events

cornerstone was impacted because cracking of the CRDM nozzles resulted in an

increase in the likelihood of a LOCA.

Enforcement: Davis-Besse TS, "Limiting Condition for Operation for Reactor Coolant

System Operational Leakage," Paragraph 3.4.6.2, stated, in part, that RCS leakage

shall be limited to no pressure boundary leakage, and that with any pressure boundary

Enclosure

104

leakage, the unit was to be in cold shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. This issue was properly

addressed by the licensees CAP; however, corrective actions were only one of the

inputs into the final characterization and resolution of this item. The NRCs investigation

into the cause of this AV, which was referred to the Office of Investigations (OI), is still

ongoing. The results of that investigation will be factored into the final enforcement

deliberations. As a result, this item remains open.

.2

(Discussed) AV 05000346/2003016-02: Reactor Vessel Head Boric Acid

Deposits

Introduction: The NRC team examined corrective actions for three AVs involving failure

to take appropriate corrective actions for continuing or recurrent deficiencies associated

with boric acid deposits on the reactor vessel head, boric acid deposits on the CACs,

and clogging of radiation element filters.

Description: The team determined that these AVs were a product of the licensees

cultural and programmatic breakdowns. To understand the licensees approach to

correcting these problems, the team examined the licensees root cause analysis report

on failure to identify significant degradation of the reactor pressure vessel head. The

causal factors for these issues were addressed in the root cause report and included:

Less than adequate safety focus;

Less than adequate implementation of the CAP; and

No safety analysis performed for the existing condition.

Corrective actions for the cultural failure associated with the inadequate safety focus

were addressed by globally by the licensees management and human performance

improvement plan and the program compliance plan. These were spelled out as

corrective actions to CR 02-00891. Among the corrective actions for these safety

culture issues were:

Corrective Action 22: Development of a management field

presence/involvement plan to improve management oversight;

Corrective Action 41: Formal assessment of the safety conscious work

environment at the plant based on criteria and attributes derived from NRC policy

and guidance;

Corrective Action 42: Changes in corporate and plant senior management;

Corrective Action 45: Development of a management monitoring process to

monitor and trend the performance of specific management oversight activities;

Corrective Action 46: Case study training for site personnel to include how the

event happened, what barriers broke down, and what must be different in the

future;

Enclosure

105

Corrective Action 74: Realignment of management incentives to place more

reward for safety and safe operation of the station; and

Corrective Action 75: Establish corporate-wide policy emphasizing the stations

industrial and nuclear safety philosophy.

Corrective actions for the failure to properly implement the CAP or to perform requisite

safety analyses were specified under CR 02-00891. These directed a complete

overhaul and re-institution of the CAP. To ensure that safety analyses were performed

as needed, corporate standards for analyses of safety issues were established and the

use of a safety precedence sequence for root cause analyses was mandated. This was

confirmed by the team and considered adequate.

The root cause report also identified other, more discrete, issues associated with these

AVs. These included:

Addressing symptoms rather than causes;

Performing less than adequate cause determinations; and

Having less than adequate corrective actions.

These were also addressed through corrective actions associated with CR 02-00891.

Some of the corrective actions included a case study of this event with an emphasis on

the need to find and address the causes of adverse conditions and the potential

consequences of failure to do so, implementation of the CARB to assess adequacy of

actions and enforce higher standards for cause evaluations and corrective actions,

mandating the use of formal root cause techniques coupled with independent reviews

and self-assessments of cause evaluations, and improvements in effectiveness reviews

with emphasis on verifying that causes have been properly addressed. These were

confirmed by the team.

The NRCs assessment of the licensees effectiveness in implementing the revised CAP

and the specific actions noted above is discussed in Sections 4OA2 and 4OA3 of this

report.

Analysis: This issue represented a performance deficiency because the licensee failed

to properly address, either individually or collectively, the cause for the continuing

accumulation of large amounts of boric acid on the reactor head, the recurrent

deposition of boric acid on CAC fins, and the repeated clogging of radiation element

filters. This lack of adequate corrective action on the licensees part contributed to their

failure to detect existing through-wall CRDM nozzle cracks and the reactor pressure

vessel head corrosion. This finding is more than minor because it affected the initiating

events cornerstone objective in that cracking of CRDM nozzles represented an increase

in the likelihood of a LOCA. The barrier integrity cornerstone was also affected in that

CRDM cracks resulted in leakage through the RCPB.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that

conditions adverse to quality be promptly identified and corrected, commensurate with

Enclosure

106

their safety significance. Criterion XVI also requires that, for significant conditions

adverse to quality, the measures assure that the cause of the condition is determined

and that corrective actions were taken to preclude repetition.

The team determined that the failure to properly address the continuing accumulation of

large amounts of boric acid on the reactor head, the recurrent deposition of boric acid

on CAC fins, and the repeated clogging of radiation element filters, significant conditions

adverse to quality, contributed to the corrosion of the reactor head. These issues have

been properly addressed by the licensees CAP; however, corrective actions were only

one of the inputs into the final resolution of this item.

The NRCs investigation into the cause of this AV, which was referred to OI, is still

ongoing. The results of that investigation will be factored into the final enforcement

deliberations. As a result, these items remain open.

.3

(Discussed) AV 05000346/2003016-03: Containment Air Cooler Boric Acid

Deposits

This issue is included as part of the discussion in Section 4OA5(1)b.4.2 above.

.4

(Discussed) AV 05000346/2003016-04: Radiation Filter Element Deposits

This issue is included as part of the discussion in Section 4OA5(1)b.4.2 above.

.5

(Discussed) AV 05000346/2003016-05: Service Structure Modification Delay

Introduction: The NRC team examined corrective actions for the licensees failure to

implement a modification that would have permitted complete inspection and cleaning of

the reactor vessel head and control rod drive mechanism nozzles.

Description: This issue addressed the licensees repeated deferral of the modification to

install multiple access ports in the service structure to permit cleaning and inspection of

the reactor head. Modification 90-0012 was initiated in March 1990 to accomplish this

but was deferred twice and then canceled in 1993. The modification was reinitiated in

May 1994 as 94-0025 and subsequently deferred four times before the head

degradation was identified in 2002.

The licensee resolved one portion of the issue through installation of the modification.

The repeated deferral was broadly addressed through the management and human

performance improvement plan and the program compliance plan as part of the

licensee's itinerary to improve safety culture. The specific issue of deferring

modifications for economic reasons was addressed by corrective actions under

CR 02-00891 for a revision to the PRC charter. The revision incorporated a requirement

to include nuclear safety in the considerations when reviewing a plant modification.

Analysis: This issue represented a performance deficiency because the licensee failed

to take corrective action (install the access port modification) for a condition adverse to

quality. As of February 16, 2002, the modification had not been performed, the head

had not been completely inspected, and the head had not been completely cleaned.

Enclosure

107

This lack of action on the licensees part, contributed to their failure to detect existing

through-wall CRDM nozzle cracks.

This finding is more than minor because it affected the initiating events cornerstone

objective in that cracking of CRDM nozzles represented an increase in the likelihood of

a LOCA. The barrier integrity cornerstone was also affected in that CRDM cracks

resulted in leakage through the RCPB. Furthermore, the failure to provide for adequate

inspection and cleaning of the head was a contributing factor to the head degradation.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that

conditions adverse to quality be promptly identified and corrected. Criterion XVI also

requires that for significant conditions adverse to quality, the measures shall assure that

the cause of the condition is determined and that corrective actions were taken to

preclude repetition.

The licensee failed to correct the condition identified on April 21, 1996 (inability to fully

inspect the head and CRDM nozzles), in that, as of February 16, 2002, the corrective

action (modification of the service structure) had not been accomplished. Although

corrective actions were completed prior to the end of the inspection, corrective actions

were only one of the inputs into the final characterization and resolution of this item.

The NRCs investigation into the cause of this AV, which was referred to OI, is still

ongoing. The results of that investigation will be factored into the final enforcement

deliberations. As a result, this item remains open.

.6

(Discussed) AV 05000346/2003016-06: Reactor Coolant System Unidentified

Leakage Trend

Introduction: The NRC team examined corrective actions for a finding involving failure

to follow the corrective action procedure and complete a prescribed corrective action for

adverse trends in RCS unidentified leakage.

Description: This URI addressed the licensees cancellation of a Mode 3 walkdown that

was the proposed corrective action for an adverse trend in RCS unidentified leakage.

Several months prior to the shutdown for the 2002 refueling outage the licensee had

been examining increases in RCS leakage and as part of an extensive investigation, a

walkdown of the containment while the plant was at NOP/NOT had been specified. The

reason for canceling the walkdown was schedule-driven; a special Mode 3 walkdown

would have delayed cooldown and entry into the lower modes required to begin

refueling.

The team concluded that the root cause for this was the licensees cultural and

programmatic breakdowns. The licensees root cause analysis report pointed to the

following causal factors:

Less than adequate safety focus;

Less than adequate implementation of the CAP; and

Less than adequate corrective actions.

Enclosure

108

Corrective actions for the cultural failure associated with the inadequate safety focus

were addressed globally by the licensees management and human performance

improvement plan and the program compliance plan and are discussed in Section

4OA5(1)b.4.2 above. Corrective actions for the failure to properly implement the CAP

were specified under CR 02-00891. These directed a complete overhaul and

re-institution of the CAP. The NRCs assessment of the licensees effectiveness in

implementing the revised CAP and the specific actions noted above is discussed in

Sections 4OA2 and 4OA3 of this report.

Analysis: This issue represented a the licensee performance deficiency because

elimination of a key component of what was an adequate proposed corrective action

rendered the proposal inadequate. Consequently, this was considered a finding

because it was reflective of other corrective action deficiencies which contributed to the

cavity in the reactor vessel head. This finding was of more than minor safety

significance because the corrosion of the reactor head and the resulting cavity

represented a significant loss of the design basis barrier integrity.

Enforcement: The licensee failed to follow the corrective action procedure and

implement an effective corrective action for adverse trends in RCS unidentified leakage.

Although corrective actions have now been completed, corrective actions were only one

of the inputs into the final characterization and resolution of this item.

The NRCs investigation into the cause of this finding, which was referred to OI, is still

ongoing. The results of that investigation will be factored into the final enforcement

deliberations. As a result, this item remains open.

.7

(Discussed) AV 05000346/2003016-07: Inadequate Boric Acid Corrosion

Control Program Procedure

Introduction: The NRC team examined corrective actions for the licensees failure to

have a BACC program procedure appropriate to the circumstances.

Description: The AIT follow-up inspection and the licensees root cause report identified

multiple deficiencies in the licensee's BACC program procedure which contributed to the

degradation of the reactor head. As part of the licensees program compliance plan, the

BACC program procedure was completely revised and subjected to a phase 2 PRB

review. The program compliance plan, the PRC review, and the revised BACC program

procedure were inspected and accepted by NRC; this inspection was documented in IR 05000346-03-09;05000346-03-11.

Analysis: This issue represented a the licensee performance deficiency because the

weaknesses in the procedure contributed to the failure, over a period of years, by the

licensees engineering staff to properly identify and evaluate the leaking CRDM nozzle

and the expanding cavity in the reactor head. This finding is more than minor because it

affected the initiating events cornerstone objective in that cracking of CRDM nozzles

represented an increase in the likelihood of a LOCA. The barrier integrity cornerstone

was also affected in that CRDM cracks resulted in leakage through the RCPB.

Enclosure

109

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, states, in part, that

activities affecting quality shall be prescribed by documented instructions, procedures,

or drawings, of a type appropriate to the circumstances and shall be accomplished in

accordance with these instructions, procedures, or drawings.

NG-EN-00324, "Boric Acid Corrosion Control Program," Revisions 0 through 2, were

classified as a quality procedure under the licensees procedure administrative system

and were not appropriate to the circumstances in that deficiencies in the procedure

contributed to the failure to detect and address corrosion of the reactor head. Although

corrective actions have now been completed, corrective actions were only one of the

inputs into the final characterization and resolution of this item.

The NRCs investigation into the cause of this AV, which was referred to OI, is still

ongoing. The results of that investigation will be factored into the final enforcement

deliberations. As a result, this item remains open.

.8

(Discussed) AV 05000346/2003016-08: Failure to Follow Boric Acid Corrosion

Control Program Procedure

Introduction: The NRC team examined corrective actions for two AVs involving failure to

follow the boric acid corrosion control program procedure and the corrective actions

program procedure.

Description: These URIs involved failure by the licensee engineering staff to follow:

A number of requirements of the BACC program procedure, most notably the

requirement to remove all boric acid and examine the base metal underneath for

signs of corrosion; and

The guidance and examples for characterization of CRs as significant, important,

routine, or non-conditions adverse to quality and, as a result, repeatedly

mis-characterized the conditions on the reactor head as routine.

The team reviewed the sections of the licensees root cause report which acknowledged

these two issues, the section of the root cause report which outlined corrective actions,

and the corrective action specified under CR 02-00891. To correct the failure to follow

the boric acid corrosion control program procedure, the licensee developed these

specific actions:

Provide training to applicable personnel and mangers on the need to remove

boric acid from components, to inspect for signs of corrosion, and to perform

inspections for signs of boric acid in component internals; and

Reinforce standards and expectations for procedure compliance and the need

for work practice rigor.

These were part of the licensees global approach to the safety culture issue as part of

the management and human performance improvement plan and the program

compliance plan.

Enclosure

110

In the root cause, the licensee acknowledged that CRs associated with the reactor head

and other boric acid conditions were categorized as relatively low, which resulted in the

use of superficial cause analysis techniques. To address this, the licensee developed

two corrective actions:

Establish and ensure that criteria for categorization of the significance of repeat

equipment failures were appropriate and used by station personnel. Criteria

were to be sufficient to elevate repeat problems to higher levels, which require

use of more robust analyses; and

Review existing long-standing issues for possible elevation to significant

condition status, thus engaging formal root cause evaluation techniques to

obtain resolution of the issues.

As part of the program compliance inspection and the corrective actions team

inspection, both of these actions were verified to have been satisfactorily completed.

Analysis: This issue represented a performance deficiency because the recurrent

failures, by the licensees engineering staff, to follow the BACC program and CAP

procedures resulted in the perpetuation of the CRDM nozzle leak and the development

of the expanding cavity in the reactor head. This finding was of more than minor safety

significance because the cavity in the reactor vessel head represented a loss of the

design basis barrier integrity.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V states, in part, that

activities affecting quality shall be prescribed by documented instructions, procedures,

or drawings, of a type appropriate to the circumstances and shall be accomplished in

accordance with these instructions, procedures, or drawings.

The licensees engineering staff failed, on multiple occasions, to adhere to both the

BACC program and the CAP procedures. Although corrective actions have now been

completed, corrective actions were only one of the inputs into the final characterization

and resolution of this item.

The NRCs investigation into the cause of this AV, which was referred to OI, is still

ongoing. The results of that investigation will be factored into the final enforcement

deliberations. As a result, this item remains open.

.9

(Discussed) AV 05000346/2003016-09: Failure to Follow Corrective Action

Program Procedure

This item is included as part of the discussion in Section 4OA5(1)b.4.8 above.

(2)

Closure of Restart Checklist Items

.1

Restart Checklist Item 2.c: Structures, Systems, and Components Inside

Containment

As part of the corrective actions resulting from the reactor vessel head degradation, the

licensee established a return to service plan to identify, monitor, and control all actions

Enclosure

111

necessary for the safe and reliable return to service of Davis-Besse. The plan consisted

of seven building blocks designed to support safe and reliable restart of the plant and to

ensure sustained performance improvements. One of the building blocks, "Containment

Extent of Condition Program," was tasked with evaluating and dispositioning the extent

of condition throughout the RCS and containment systems, structures, and components

relative to the degradation mechanisms that occurred on the reactor vessel head.

IR 05000346/2002009 reviewed the licensees plan for inspections, including methods,

control of walkdown boundaries, resolution of obstructed examinations, and control of

inspection records. Two findings of very low safety significance were identified. The

first was associated with lack of acceptance criteria and the second was associated with

inadequate training and certification of inspection personnel. Weaknesses were

identified in the licensees implementation of the containment inspection program.

IR 05000346/2002012 focused on evaluating corrective actions for the issues previously

identified. This inspection concluded that the above issues were adequately resolved

and that the inspections were effectively implemented. Three URIs associated with

corrective actions for corrosion of electrical conduit, potential leakage of reactor vessel

bottom head incore instrumentation penetrations, and failure to follow the procedure for

Raychem' splice removal on electrical cable were identified. Restart Checklist Item 2.c

was held open pending review of these URIs.

Unresolved item 05000346/2002012-01 was discussed and closed in IR 05000346-03-23. The NRC reviewed the licensees activities to resolve the potential

leakage of reactor vessel bottom head incore instrumentation penetrations. The

licensee performed chemical analysis of the deposits found on the reactor vessel sides

and bottom, and in a July 30, 2003, letter to the NRC, concluded that the deposits did

not result from leakage from the penetrations. Additionally, the bottom head was

inspected for signs of leakage after completion of the seven day NOP/NOT leak test.

This test provided reasonable assurance that the bottom head penetrations were not

leaking.

Unresolved item 05000346/2002012-02 concerning corrosion of electrical conduit is

discussed and closed in Section 4OA5(1)b.1.1 of this report.

Unresolved item 05000346/2002012-03 concerning removal of Raychem' splices from

electrical cable is discussed in Section 4OA3(2)b.6 and the URI is closed in Section

4OA5(1)b.1.2.

On November 18, 2003, the Davis-Besse Oversight Panel met to discuss this issue and

concluded that Restart Checklist Item 2.c is closed.

.2

Restart Checklist Item 3.a: Corrective Action Program

As part of the corrective actions resulting from the reactor vessel head degradation, the

licensee established a return to service plan to identify, monitor, and control all actions

necessary for the safe and reliable return to service of Davis-Besse. A key element of

the return to service plan was for the licensee to reestablish and reinvigorate the CAP to

ensure that future conditions adverse to quality were properly identified, evaluated and

Enclosure

112

corrected. The NRC performed a review of the CAP which was documented in NRC

Inspection Report Nos. 50-346/02-11 and 50-346/03-09 and found the program to be

acceptable. Restart Checklist item 3.a was left open following these inspections,

pending completion of the CATI.

The main function of the CATI inspection, described in the report above, was to evaluate

the licensees effectiveness in correcting the deficiencies in the CAP. As noted in the

previous sections of the report, the team identified numerous deficiencies still existing

within the CAP. Nevertheless, the team concluded that the licensees corrective actions

were acceptable to support plant restart.

These deficiencies were discussed with the licensee during two public meetings, one on

November 12, and a second on December 10, 2003. As part of these meetings, the

licensee made a number of commitments to further improve the CAP as part of its

Operational Improvement Plan for Cycle 14, Revision 2.

The team presented the results of this inspection to the NRC Davis-Besse Oversight

Panel on February 5, 2004. The panel concluded that, based upon the licensees

improvement plans, Restart Checklist Item 3.a could be closed.

.3

Restart Checklist Item 5.b: Systems Readiness for Restart

As part of the corrective actions resulting from the reactor vessel head degradation, the

licensee established a return to service plan to identify, monitor, and control all actions

necessary for the safe and reliable return to service of Davis-Besse. One of the key

elements of this return to service plan was a systematic review of a number of

safety-related systems.

Concurrent with the licensees initial evaluation of the systems, the NRC performed a

SSDI as documented in IR 05000346/2002014. This inspection identified a large

number of NCVs and URIs which required resolution to ensure system operability prior

to restart. As part of this inspection effort, the team evaluated the adequacy of the

licensees corrective actions to address and resolve the identified deficiencies.

The teams findings and conclusions documented in this report revealed weaknesses in

the licensees implementation of corrective actions and in the engineering rigor to

address and resolve identified deficiencies. Throughout the inspection, the team also

made observations and reached conclusions regarding the safety significance of the

identified deficiencies and ability of affected components to perform the intended design

function. Concerns and issues were presented to the licensee for entry into their

corrective action program and final implementation of corrective actions. The teams

inspection did not reach a conclusion regarding the readiness of systems to support

restart since during the teams inspection, the licensee was still in the process of

returning systems to functional and operational status. Therefore, restart checklist item

5.b remains open, and will be further addressed in a separate NRC inspection report.

Enclosure

113

4OA6 Management Meetings

Exit Meeting Summary

The team presented the inspection results to Mr. L. Myers and other members of

licensee management and staff at the conclusion of the inspection on September 9,

2003. The licensee acknowledged the information presented.

Per the licensees request, on November 10, 2003, the team presented the latest

inspection results, during a telephone conference, to Mr. L. Myers and other members of

the licensee management and staff. The licensee acknowledged the information

presented.

On January 7, 2004, the team held a telephone exit with the licensee in regard to the

HPI minimum flow issue discussed in Section 4OA3(3)b.1.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Bezilla, Site Vice President

B. Boles, Manager, Plant Engineering

K. Byrd, Supervisor, Design Engineering

L. Dohrmann, Manager, Performance Improvement

J. Grabnar, Manager, Design Engineering

L. Griffith, Manager, Employee Concern Program

D. Gudger, Supervisor, Regulatory Affairs

J. Hagan, Senior Vice President, FENOC

G. LeBlanc, Supervisor, Design Engineering

S. Loehlein, Manager, Nuclear Quality Assurance

W. Marini, Regulatory Interface

M. Marler, Training Manager

L. Myers, Chief Operating Officer, FENOC

K. Ostrawski, Manager, Regulatory Affairs

W. Pearce, Vice President, Oversight

J. Powers, Director, Nuclear Engineering

C. Price, Manager, Business Services

J. Rinckez, Director, Nuclear Fuel

R. Schrauder, Director, Support Services

L. Strauss, Analyst, Regulatory Affairs

J. Sturdavant, Regulatory Affairs

Nuclear Regulatory Commission

R. Gardner, Senior Project Manager, Division of Reactor Safety

J. Grobe, Chairman, Davis-Besse Oversight Panel

J. Lara, Branch Chief, Electrical Engineering Branch, Division of Reactor Safety

C. Lipa, Chief, Reactor Projects Branch 4

W. Ruland, Senior Project Manager, NRR

J. Rutkowski, Resident Inspector

S. Thomas, Senior Resident Inspector

Attachment

A2

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000346/2003010-01

VIO

Failure to Take Corrective Actions for a Previous NCV

Concerning SW Discharge Path Swapover Setpoints

(Section 4OA3(3)b.11)05000346/2003010-02

VIO

Failure to Take Corrective Actions for a Previous NCV

Concerning SW Pump Discharge Check Valve

Acceptance Criteria (Section 4OA3(3)b.12)

Open and Closed in This Report

05000346/2003010-03

NCV

Undervoltage Time Delay Relay Setting Did Not Account

For Instrument Uncertainties (Section 4OA3(2)b.1)05000346/2003010-04

NCV

Lack of 480 Vac Class 1E Motor Thermal Overload

Protection (Section 4OA3(2)b.2)05000346/2003010-05

NCV

Failure to Perform Adequate Direct Current Contactor

Testing to Ensure Minimum Voltage at Motor Operated

Valves (Section 4OA3(2)b.3)05000346/2003010-06

NCV

Failure to Verify Adequacy of Short Circuit Protection for

Direct Current Circuits (Section 4OA3(2)b.4)05000346/2003010-07

NCV

Lack of Calculations to Ensure Minimum Voltage

Availability at Device Terminals (Section 4OA3(2)b.5)05000346/2003010-08

NCV

Failure to Verify Adequacy of HPI Minimum Recirculation

Line Design (Section 4OA3(3)b.1)05000346/2003010-09

NCV

Increased Dose Consequences Due to Degraded Thermal

Performance Operation of Degraded CAC (Section

4OA3(3)b.2)05000346/2003010-10

NCV

Containment Air Cooler Air Flow Calculation Concerns

(Section 4OA3(3)b.3)05000346/2003010-11

NCV

Accumulator Sizing Calculation Errors (Section

4OA3(3)b.4)05000346/2003010-12

NCV

Non-conservative Calculation Used in Design Analysis to

Determine Required Service Water Makeup Flow to

Component Cooling Water (Section 4OA3(3)b.6)05000346/2003010-13

NCV

Calculation Concerns for Service Water Pump Room

Ventilation System (Section 4OA3(3)b.7)

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont

Attachment

A3

05000346/2003010-14

NCV

Inadequate Service Water System Flow Analysis (Section

4OA3(3)b.8)05000346/2003010-15

NCV

Inadequate Flooding Protection for the Service Water

System (Section 4OA3(3)b.9)05000346/2003010-16

NCV

Inadequate Service Water System Flow Balance Testing

Procedure (Section 4OA3(3)b.10)05000346/2003010-17

NCV

Lack of Design Basis Calculations to Support Service

Water Valve Single Failure Assumptions (Section

4OA3(3)b.13)05000346/2003010-18

NCV

Auxiliary Feedwater System Calculation Issues With Main

Steam Safety Valves (Section 4OA3(3)b.14)05000346/2003010-19

NCV

Preconditioning of Auxiliary Feedwater System During

Testing (Section 4OA3(3)b.15)05000346/2003010-20

NCV

Borated Water Storage Tank Calculation Issues (Section

4OA3(3)b.18)05000346/2003010-21

NCV

Inadequate Evaluation of Reactor Coolant Pump

Casing-to-cover Stud Overstressing (Section

4OA3(3)b.19)05000346/2003010-22

NCV

ECCS Motors Not Qualified for Service Time (Section

4OA3(3)b.21)05000346/2003010-23

NCV

Inappropriate Application of 10 CFR 50.59 (Section

4OA3(3)b.23)05000346/2003010-24

NCV

Failure to Perform Comprehensive Moderate Energy Line

Break Analysis (Section 4OA3(3)b.24)05000346/2003010-25

NCV

Repetitive Spacer Grid Strap Damage (Section 4OA3(4)b)05000346/2003010-26

NCV

Process Monitoring Function for Alternative Shutdown

Capability (Section 4OA3(5)b.1)05000346/2003010-27

NCV

Supporting Functions for Alternative Shutdown Capability

(Section 4OA3(5)b.2)05000346/2003010-28

NCV

Emergency Diesel Generator Floor Drains Design

Deficiency (Section 4OA3(5)b.3)

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont

Attachment

A4

05000346/2003010-29

NCV

Failure to Provide HPI Recirculation Line (Section

4OA3(6)b.3)

Closed

05000346/2002-009-00

LER

Degradation of the High Pressure Injection Thermal

Sleeves05000346/2002012-02

URI

Potential Impact of Corrosion on the Ground Function of

Electrical Conduit in Containment

05000346/2002012-03

URI

Potential Failure to Follow the Procedure for Raychem'

Splice Removal on Electrical Cables

05000346/2002014-01c

URI

Failure to Perform Comprehensive Moderate Energy Line

Break Analysis

05000346/2002014-01d

URI

Lifting of Service Water Relief Valves

05000346/2002014-01e

URI

Inadequate Service Water Pump Room Temperature

Analysis

05000346/2002014-01f

URI

Inadequate Service Water Pump Room Steam Line Break

Analysis

05000346/2002014-01g

URI

Inadequate Cable Ampacity Analysis

05000346/2002014-01h

URI

Inadequate Flooding Protection for Service Water Pump

House

05000346/2002014-01j

URI

Poor Quality Calculation for 90 Percent Undervoltage

Relays

05000346/2002014-01l

URI

Inadequate Calculations for Control Room Operator Dose

(GDC-19) and Offsite Dose (10 CFR Part 100) Related to

High Pressure Injection (HPI) Pump Minimum Flow Values

05000346/2002014-01m

URI

Other GDC-19 and 10 CFR Part 100 Issues

05000346/2002014-01n

URI

High Pressure Injection Pump Operation Under Long Term

Minimum Flow

05000346/2002014-01o

URI

Some Small Break Loss of Coolant Accident Sizes Not

Analyzed

05000346/2002014-01p

URI

Inadequate Service Water System Flow Analysis

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont

Attachment

A5

05000346/2002014-01q

URI

Inadequate Service Water System Thermal Analyses

05000346/2002014-01r

URI

Inadequate Ultimate Heat Sink Inventory Analysis05000346/2002014-01s

URI

No Valid Service Water Pump Net Positive Suction Head

Analysis

05000346/2002014-01t

URI

Service Water Source Temperature Analysis for Auxiliary

Feedwater

05000346/2002014-01u

URI

Inadequate Short Circuit Calculations

05000346/2002014-02b

URI

Inadequate Service Water System Flow Balance Testing

05000346/2002014-03a

URI

Inappropriate Service Water Pump Curve Allowable

Degradation

05000346/2002014-03b

URI

Repetitive Failures of Service Water Relief Valves

05000346/2002014-03c

URI

Non-conservative Difference in Ultimate Heat Sink

Temperature Measurements

05000346/2002014-03e

URI

Non-conservative Containment Air Cooler Mechanical

Stress Analysis05000346/2002014-05

URI

Question Regarding the Definition of a Passive Failure

05000346/2002019-031

URI

Final Evaluation of Apparent Cause Evaluation for LER 05000346/2002-06-00

05000346/2003-03-00

LER

Potential Inadequate High Pressure Injection Pump

and -01

Minimum Recirculation Flow Following a Small Break Loss

of Coolant Accident

Discussed

05000346/2002-08-00

LER

Containment Air Coolers Collective Significance of

and -01

Degraded Conditions

05000346/2002014-01a

NCV

Lack of a Design Basis Analysis for Containment Isolation

Valve Backup Air Supplies

05000346/2002014-01b

NCV

Inadequate Blowdown Provisions for CAC Backup Air

Accumulators

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED, cont

Attachment

A6

05000346/2002014-01i

NCV

Non-conservative TS Value for 90 Percent Undervoltage

Relays

05000346/2002014-01k

NCV

Non-conservative Relay Setpoint Calculation for the 59

Percent Undervoltage Relays

05000346/2002014-01v

NCV

No Analytical Basis for Setpoint to Swap Service Water

System Discharge Path

05000346/2002014-02a

NCV

SW Surveillance Test Did Not Use Worst Case Values

05000346/2002014-03d

NCV

Inadequate Corrective Actions Related to SW Pump

Discharge Check Valve Acceptance Criteria

05000346/2002014-04

NCV

Failure to Perform TS Surveillance Requirement for HPI

Pump Following Maintenance

05000346/2003016-01

AV

Reactor Operation with Pressure Boundary Leakage (URI

05000346/2002008-01)

05000346/2003016-02

AV

Reactor Vessel Head Boric Acid Deposits (URI

05000346/2002008-02)

05000346/2003016-03

AV

Containment Air Cooler Boric Acid Deposits (URI

05000346/2002008-03)

05000346/2003016-04

AV

Radiation Element Filters (URI 05000346/2002008-04)

05000346/2003016-05

AV

Service Structure Modification Delay (URI

05000346/2002008-05)

05000346/2003016-06

AV

Reactor Coolant System Unidentified Leakage Trend (URI

05000346/2002008-06)

05000346/2003016-07

AV

Inadequate Boric Acid Corrosion Control Program

Procedure (URI 05000346/2002008-07)

05000346/2003016-08

AV

Failure to Follow Boric Acid Corrosion Control Program

Procedure (URI 05000346/2002008-08)

05000346/2003016-09

AV

Failure to Follow Corrective Action Program Procedure

(URI 05000346/2002008-09)

Attachment

A7

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC team reviewed the documents in their entirety but rather that selected

sections of portions of the documents were evaluated as part of the overall inspection effort.

Inclusion of a document on this list does not imply NRC acceptance of the document or any part

of it, unless this is stated in the body of the inspection report.

Bulletins 88-04; Potential Safety-Related Pump Loss; May 5, 1988

03-01; Potential Impact of Debris Blockage on Emergency Sump Recirculation at

Pressurized-Water Reactor; June 9, 2003

Calculations

C-CSS-009.03-002; Assessment of Safety Related Structures from the Effects of Intake

Structure Gantry Fall During a Tornado Event; Revision 0

C-CSS-099.20-026; Probability of Tornado Missile Damage to Davis-Besse Missile

Exposed Targets; Revision 1; January 6, 2003

C-EE-002.01-010; Battery Load Profile; Revision 29; September 18, 2002

C-EE-004.01-049; 4.16 kV Bus Degraded (90 Percent Undervoltage) Relay Setpoint

Relay Setting Table Bus C1; Revision 2

C-EE-004.01-049; 4.16 kV Bus Degraded (90 Percent Undervoltage) Relay Setpoint

Relay Setting Table Bus D1; Revision 7

C-EE-015.03-008; Electric Transient Analysis Profile; Revisions 0 and 2

C-EE-024.01-008; Evaluation of Davis-Besse EDG Voltage Frequency Response During

Design Basis LOOP/LOCA Transient Loading MPR 0200-0049-08-01; Revision 1

C-ICE-011.01-002; Service Water Flow/Pressure Indications; Revision 0

C-ICE-048.01-004; SFAS BWST Low Level Setpoint; Revision 7; April 22, 2003

C-ME-011.01-131; Service Water Relief Valve Setpoint and Capacity; Revision 0;

Addendum A01

C-ME-011.01-137; Service Water Pump NPSH; Revision 0

C-ME-011.01-140; SW/CCW Makeup Line 1 HBC-35 Flow Rate; Revision 0;

March 6, 2003

Attachment

A8

C-ME-011.06-007; Accumulator Sizing for Service Water Valves SW1356, SW1357 and

SW1358; Revisions 0, 1, and 2

C-ME-024.02-002; Maximum Outside Temperature for EDG Operability; Revision 1;

April 2, 2002

C-ME-030.01-008; Operability for Rooms 323, 324, and 325 with Loss of Normal

Ventilation; Revision 0; February 4, 2003

C-ME-060.05-003; TP 850.31.01 Acceptance Criteria; Revision 0; November 13, 1986

C-ME-060.05-014; Containment Air Cooler System Fan Performance; Revision 0;

September 9, 2003

C-NSA 000.00-017; PROTO-FLO Service Water System Model; December 19, 2001

C-NSA 000.00-019; GOTHIC Model Inputs for DB Primary Containment; Revision 0;

February 4, 2003

C-NSA 011.01-010; Maximum Service Water Pressure to AFW System; Revision 0;

April 2, 2002

C-NSA-032.02-006; ECCS Pump Room Heatup During Post LOCA; Revisions 0 and 1

C-NSA-040.01-006; TSP Volume Increase due to RCS Leakage; Revision 1;

November 4, 2002

C-NSA-050.03-009; Auxiliary Feedwater Flow as a Function of Decay Heat; Revision 0

C-NSA-050.03-013; Auxiliary Feedwater System Curve; Revision 1

C-NSA-050.03-015; Auxiliary Feedwater Pump Turbine Steam Pressure Drop and Low

End Pump Operation; Revisions 2 and 3

C-NSA-050.03-022; Acceptance Criteria for Auxiliary Feed Pump Quarterly Surveillance

Test; Revision 2

C-NSA-050.03-023; Auxiliary Feedwater Pump Turbine Operation with Open or Broken

11/2-Inch Minimum Flow Line for Modification 95-060; Revisions 0 and 1

C-NSA-059.01-019; Water Level Inside Containment Post-LOCA; Revision 2;

March 28, 2003

C-NSA-060.05-008; Containment Post LOCA Response with Variable SW Temperature;

Revision 3; October 20, 2001

C-NSA-060.05-010; Containment Analysis; Revision 2; February 1, 2003

Attachment

A9

E-ECS-099.16-146; Thermal Aging Effect of ECCS Room Post LOCA Temperature;

Revision 0; February 26, 1992

FANP86-5024418-01 DB-1; Post-LOCA pH Analysis; Revision 1; March 19, 2003

SR-0964; Flowserve Cover Gasket Upgrade Verification for Davis-Besse Primary

Coolant Pumps; Revision 1; February 3, 2003

02-113; Service Water System Design Basis Flow Analysis; Revision A

02-123; Service Water System Model Development and Benchmark; Revision B

02-124; Service Water System NPSH; Revision A

03-011; SW System Performance Following an Appendix R Event; Revision A;

March 13, 2003

03-013; Service Water System Test Acceptance Criteria Correction Factors; Revision A

12501-00004; UHS Pond Thermal Performance; Revision 0

12501-M-002; LOCA and MSLB Containment Analysis with Increase of Allowable

Service Water Temperature to 90 Degrees F; Revision 0; January 26, 1999

12501-M-003; ECCS Pump Room Temperatures with Initial 90 Degrees F Forebay;

Revision 0; May 27, 1999

24.001; Calculated Temperature -vs.- Time in Rooms 323, 324, and 325; Revisions 1

and 3; July 24, 2003

28.003; Bechtel CAC Fan Motor; Revision 0

28.004; Containment Cooling System Pressure Drop; Revision 2; September 7, 2003

32-1171148-00; Loss of Feedwater Analysis; Revision 0

51-5023378-00; February 20, 2003

67.004; Service Water Pump Maximum Allowable Outside Air Temperature to Dissipate

Entire Room Heat Load with One Ventilation Fan C99 1, 2, 3, or 4 Operable; Revision 1

67.005; Service Water Pump Room Ventilation System Capacity; Revision 4;

November 20, 2002

67.007; Service Water Pump Room Ventilation System - Pressure Drop;

August 30, 2002

86-5007079-00; SG Over-Pressure Protection Report; Revision 0

Attachment

A10

86-5022260-00; Determination of HPI Pump Operability During Post-LOCA Sump

Recirculation For All Break Sizes And Transient Scenarios; Revision 0

86-5024418-01; DB-1 Post-LOCA pH Analysis Report; Revision 0

Condition Reports Generated as a Result of this Inspection

03-02191; Corrective Action Approval Without Supporting Documentation Finalized;

March 19, 2003

03-02195; Ambiguous Description in CRA No.8 to CR 02-07646; March 19, 2003

03-02298; Failure to Generate CR for Unresolved Issues in NRC Inspection Report;

March 19, 2003

03-02445; Incorrect Processing of CR 02-09928 and CR 02-0939; March 27, 2003

03-02475; Inadequate Blowdown Provisions for CAC Air Accumulators; March 28, 2003

03-02577; Appendix R Safe-Shutdown Concerns with EDG Floor Drains; April 1, 2003

03-02597; Bypassed Overload Heaters in Class 1E 480V Motors; April 2, 2003

03-02616; RFA - Bypassing Overload Heater Trips on 1E 480V Motors; April 2, 2003

03-02651; Framatome AFW Issues with MSSV; April 3, 2003

03-02654; Cable Ampacity on Containment Spray Pump Motor; April 2, 2003

03-02730; Lack of Vendor Data for High Voltage Switchgear at High Temperature;

March 19, 2003

03-03184; Administrative Issues with CR 02-05640; April 25, 2003

03-03572; Lack of Coordination of Protective Devices on Bus E1 and F1; May 7, 2003

03-03891; EDG Room Heater Non-Q Yet Credited in USAR; May 19, 2003

03-03977; SW Calculations Do Not Provide Sufficient Documentation of Results;

May 22, 2003

03-03979; CR 02-00891 CA-30 Operation Confidence Review Closed Out Early;

May 22, 2003

03-03980; Past CAC Operability Determination Lacks Adequate Technical Justification;

May 22, 2003

03-03986; Rating of the Containment Air Cooler Fan Motors; May 22, 2003

Attachment

A11

03-04010; NRC Review of SW/CCW Interface Calculation; May 22, 2003

03-04018; NRC Pointed out Discrepancy in Mode Hold Resolution for CR 02-01523;

May 23, 2003

03-04035; Trending CR - Timeliness of the Evaluation of SCAQ CR 02-02943;

May 22, 2003

03-04225; Response Team Communications Self-Identified During Inspection;

May 28, 2003

03-04264; Non-Q Motor Loads Without Overload Heaters; May 30, 2003

03-04303; CR 03-02597 (O/L HTR Bypass) Evaluation Concerns By NRC; June 2, 2003

03-04341; Past Operability/Reportability Review of Previous CR 03-02699;

dated June 3, 2003

03-04375; SR Potential Current Overloads on Load Center Breakers Feeding MCCs;

June 4, 2003

03-04423; Passive Failure Assumptions; June 5, 2003

03-04435; Preliminary Davis-Besse AC System Analysis Results; June 6, 2003

03-04668; No Guidance/Criteria for a Collective Significance Review; June 13, 2003

03-04684; Isolated Occurrences of Staff Not Trained to NOP-LP-2001 Revision 4;

June 13, 2003

03-05681; Inadequate Operability/Reportability Determination; July 15, 2003

03-05715; SBODG Does Not Have a Load Table; July 16, 2003

03-05739; Deficiencies in Component Evaluation for EDG Room High Temperature;

July 17, 2003

03-05917; Concern Regarding Containment Spray Pump Overload Protection;

July 23, 2003

03-05919; Concerns Regarding 480V Breaker Coordination for Appendix R Compliance;

July 23, 2003

03-05920; Basis Not Defined for all the Appendix R DC and 120 Vac Circuits;

July 23, 2003

03-06153; Timeliness of Changes to the USAR; July 31, 2003

03-06338; Discrepancies in CR 02-06773 Response; August 8, 2003

Attachment

A12

03-06375; Concerns with Motor Overload Protection for Non-Essential Service Motors;

August 8, 2003

03-06383; Revise C-ME-011.06-007 Nitrogen Bottle Sizing for SW1356, SW1357 and

SW1358; August 8, 2003

03-06418; Interdependencies of Calculations Associated with EDG Rating and Capacity

Self-Identified In Preparation for Inspection; August 9, 2003

03-06421; Lack of Corrective Action for Cause Identification CR 02-05262 Self-Identified

In Preparation for Inspection; August 9, 2003

03-06427; Lack of Corrective Action for Cause Identification CR 02-07110 Self-Identified

In Preparation for Inspection; August 9, 2003

03-06428; Lack of Corrective Action for Cause Identification CR 02-09027 Self-Identified

In Preparation for Inspection; August 9, 2003

03-06457; Discrepancies Between Quality and Seismic Classifications;

August 11, 2003

03-06458; Invalid Information Restored to Procedure During Alteration Self-Identified In

Preparation for Inspection; August 11, 2003

03-06474; Containment Spray Pump Current Values are Non-conservative;

August 11, 2003

03-06475; Evaluation of Overloads on Motor Operated Valves; August 11, 2003

03-06485; Installed Equipment Size Differs From that Shown in the Calculation;

August 12, 2003

03-06492; EDG Water Jacket Heat Exchanger PM Enhancement; August 12, 2003

03-06497; CATI: The NRC Team Disagrees With CR 03-03891 Resolution;

August 12, 2003

03-06499; Item 0292 - 50.59 Evaluation Using NRC Pre-approved Methodologies;

August 12, 2003

03-06507; Tracking CR for Actions Recommended By CR 03-04423; August 12, 2003

03-06519; Periodic Vibration Testing of LPI Pumps on Minimum Flow; August 13, 2003

03-06520; Potential Concern for Pre-Conditioning Prior to Surveillance Test;

August 13, 2003

03-06524; EDG Conduit Installation for Cabinet C3615; August 2, 2003

Attachment

A13

03-06526; Adequacy of HPI Pump Minimum Flow Rate; August 13, 2003

03-06547; Potential for Supervisor/SRO Comments to Influence CR Outcome;

August 13, 2003

03-06556; NRC Questions/Issues In AOV C-ME-011.06.007; August 14, 2003

03-06561; 50.59 Evaluation 02-01740 Concerns; August 14, 2003

03-06567; Accuracy of SRO Comments on 03-02597; August 14, 2003

03-06576; Auxiliary Feedwater Components Should be in GL89-13 Program;

August 14, 2003

03-06578; Concern Over AFW Strainer Limiting Particle Size Report; August 14, 2003

03-06585; Inaccurate Investigation of CR 02-07547 Self-Identified In Preparation for

Inspection; August 14, 2003

03-06586; Clarification to CR 02-06661; August 13, 2003

03-06588; Item 0352, LAR 96-0008 Incomplete Statements, EQ Questions;

August 14, 2003

03-06656; NSA Calculations May Not Have Been Revised Properly; August 18, 2003

03-06809; Improvements to 10 CFR 50.9 Completeness and Accuracy Training;

August 21, 2003

03-06837; Item 0375 - Potential Thermal Overpressurization of the SW Sys. to CACS;

August 22, 2003

03-06870; NRC Unresolved Issues, Concerns with SW Pump Room HVAC 67.005;

August 23, 2003

03-06901; Error Found in Flooding Calculation 15.50 Revision 1; August 25, 2003

03-06907; Quality Collective Significance Review; August 23, 2003

03-06908; Corrective Action Program Implementation Collective Significance Review;

August 23, 2003

03-06909; Design Control Collective Significance Review; August 23, 2003

03-06941; Recommended SW Balance Procedural Enhancement; August 26, 2003

03-06944; Fuse Sizing for MV0106 and MV38700; August 25, 2003

03-06948; Downgrade of CR 02-06356; August 26, 2003

Attachment

A14

03-06956; 0300 - DC Voltage Drop LC - Lack of Basis for Deferring Corrective Action;

August 26, 2003

03-06984; Questions on NOP-CC-2003, Engineering Changes; August 26, 2003

03-06989; ETAP Revision 2 Number was not Attained in Accordance with

NOP-CC-3002; August 27, 2003

03-06990; Possible Enhancement to NOP-CC-3002 as Identified During TI-0409;

August 27, 2003

03-06996; Root Cause for 02-06178 Spacer Grid Damage Needs Improvement;

August 27, 2003

03-07006; Translation of Flow Balance Acceptance Criteria Should Be Formalized;

August 27, 2003

03-07009; CAC Motor Sizing; August 27, 2003

03-07031; Inadequate Rollover from CR 03-02616 to CR 03-03572; August 28, 2003

03-07033; Inadequate Past Operability Evaluation for CR 03-03572; August 28, 2003

03-07035; Performance Improvement Involvement in MCTM; August 28, 2003

03-07042; UFSAR Needs to Be Clarified on Use of Safety Related Equip and Seismic;

August 28, 2003

03-07047; NRC Concerns with CR Evaluations Failure to Answer the Identified Issue;

August 28, 2003

03-07053; Evaluation for Operability and USAR Update Timeliness; August 28, 2003

03-07067; Observation of Proposed Service Water Relief Valve Removal EWR 01-0306;

August 29, 2003

03-07069; Adequacy of Electrical DC Contactor Testing Methodology; August 29, 2003

03-07112; Collective Significance Review of Recent Operability Evaluation Revisions;

August 28, 2003

03-07121; NRC Non-Cited Violation Issues; August 30, 2003

03-07124; NRC Concerns with CR Evaluations Not Including Applicable References;

August 30, 2003

03-07256; Questions on Applicability of 50.59 for Manual Actions in Fire Preplans;

September 2, 2003

Attachment

A15

03-07420; Restart CRs Closed Prior to All CAs Being Completed; September 6, 2003

03-07922; Thermal Overload #2 EDG Air Compressor; September 21, 2003

03-09548; New Motor Operated Valve Terminal Voltage; November 5, 2003

Condition Reports Reviewed During the Inspection

99-01109; Conversion of PCAQR 1998-0126 to Condition Report; June 28, 1999

00-00669; Potential Non-Compliance Against the ASME Code; April 1, 2000

00-00699; Steady State Leakage from Three of Four Reactor Coolant Pump Gasket

Drain Lines; April 2, 2000

00-00869; Leakage at the Bolted Connection on Reactor Coolant Pump 1-1;

April 10, 2000

00-01089; Relaxation of Reactor Coolant Pump Casing Studs since Refueling Outage

11; April 20, 2000

00-02033; Reactor Coolant System Flow Rate Test Acceptance Criteria Not Met;

August 11, 2000

00-02304; Performance of DB-SP-04360 In Modes 1 and 2; September 21, 2000

00-02418; Zebra Mussel Particles in Service Water Lines Might Restrict Flow Through

the Auxiliary Feedwater Restriction Orifices; October 6, 2000

01-00540; Dose Calculations for Post Accident Sampling System Samples Outside of

Updated Safety Analysis Report 9.3.2.2.3; February 23, 2001

01-00890; Reactor Coolant System Leak Rate Data Scatter; March 28, 2001

01-01102; Letdown Diverting Valve, MU11, Is Possible Source of Reactor Coolant

System Unidentified Leakage; April 20, 2001

01-01335; CAC Air Side Fouling Criteria; May 22, 2001

01-01857; RCS Leakage Anomalies; July 25, 2001

01-02019; Initial Results of Investigation into NRC Information Notice 2000-20;

August 7, 2001

01-02820; Procedures Not Updated to Support Modification Implementation;

October 23, 2001

01-02862; Potential Adverse Trend in Unidentified Reactor Coolant System Leakage;

October 25, 2001

Attachment

A16

01-03025; Reactor Coolant System Leakage; November 12, 2001

01-03059; Minimum Voltage for AFW Valves MV0106 and MV3870; November 2001

02-00164; ASME Relief Request for the 13th Refueling Outage; January 16, 2002

02-00412; DC Voltage Drop Calculation; February 8, 2002

02-00576; Small Oil Leak Discovered on Reactor Coolant Pump Motor 2-2;

February 18, 2002

02-00695; Latent Issues Review (LIR) - EDG Engine Derating; February, 2002

02-00835; LIR - RCS: RCS Validation Document Contains Outdated Information;

February, 2002

02-00890; Control Rod Drive Nozzle Crack Indication; February 27, 2002

02-00891; Failure to Identify Significant Degradation of the Reactor Pressure Vessel

Head (Selected Corrective Actions Only); February 2002

02-01129; Valve MU66C As-found Close Stroke Time Exceeded Maximum Allowable;

February 2002

02-01139; Corrosion of Containment Air Cooler 3 Flange Faces; March 8, 2002

02-01517; Containment Inspection Plan Not Fully Implemented; April 10, 2002

02-01523; Reactor Coolant Pump 1-1 and 1-2 Leakage at Gasket Drain Lines;

February 16, 2002

02-01691; Inspection Plan IP-M-028 Findings; April 25, 2002

02-01915; Inspection Plan IP-M-028 (Extent of Condition) Examination Findings;

May 6, 2002

02-02143; Inspection Plan IP-M-028 (Extent of Condition) Examination Findings;

May 17, 2002

02-02419; Untimely Corrective Action to Address Corrective Action Program

Weaknesses; June 4, 2002;

02-02584; Implementation of Corrective Action Program by Site Personnel;

June 13, 2002

02-02585; Management and Supervisory Oversight and Ownership of Plant Activities;

June 13, 2002

02-02658; Inadequate Ventilation for Rooms 323, 324 and 325

Attachment

A17

02-02848; Fuel Assembly Spacer Grid Impressions in Core Baffle Plates; June 27, 2002

02-02943; Containment Air Cooler Boric Acid Corrosion; July 2, 2002

02-03027; Emergency Diesel Generator Jacket Water Heat Exchanger Tubeside (CCW)

Flow Rates Exceed Limits; July 8, 2002

02-03157; High Energy Line Breaks in Turbine Building Effects on AFW Pump Rooms;

July 11, 2002

02-03337; Documentation Could Not be Located; July 19, 2002

02-03497; Overall Failure to Take Action to Correct Identified Deficiencies in CAP;

July 27, 2002

02-03674; Recurring Trend of Untimely and Ineffective Corrective Actions;

August 3, 2002

02-03668; Reactor Coolant Pump Casing-to-cover Joint Leakage; August 3, 2002

02-03673; Recurring Trend of Less Than Adequate CR Evaluations; August 3, 2002

02-03674; Recurring Trend of Untimely and Ineffective Corrective Actions; August 3

2002

02-03676; Coding and Trending; August 3, 2002

02-03960; CAC Operability; August 9, 2002

02-03963; Zebra Muscle Shells in Containment Air Cooler Cooling Coils; August 9, 2002

02-04083; LIR - EQ: 36 inch Main Steam Line Analysis; August 10, 2002

02-04146; EDG 2 Missile Shield Support Plates Have Broken and Cracked Concrete;

August 11, 2002

02-04147; Missile Protection on Stacks about Six Feet Short of Completely Effective;

August 11, 2002

02-04202; Oxidation on Fuses and Fuse Holders; August 12, 2003

02-04211; Performance Indicator Weakness Collective Review; August 14, 2002

02-04292; Inadequate Cause Evaluations and Corrective Actions; August 15, 2002

02-04630; LIR - Emergency Diesel Generator 1-2; August 18, 2002

02-04668; LIR - AFW-EQ Equipment Sealing; August 21, 2002

Attachment

A18

02-04673; Auxiliary Feedwater Strainers Limiting Particle Size; August 22, 2002

02-04680; No Documentation To Assure Compliance With GE SIL-44 For HFAs;

August 21, 2002

02-04700; Tornado Missile Protection; August 21, 2002

02-04716; Recurring Trend of Procedural Non-Compliance; August 21, 2002

02-04740; Refer to DB-OP-01200 for Step Changes in Unidentified RCS Leakage;

August 22, 2002

02-04810; LIR - AFW-W-PSL 4929A and B; August 17, 2002

02-04884; Ineffective Corrective Action Problem Resolution; August 23, 2002

02-05039; LIR - EDG System Does Not Meet IEEE-STD-387-1972 Requirements;

August 26, 2002

02-05079; LIR - AFW-SFRCS High Level Isolation; August 26, 2002

02-05096; Reinspection of RCP21OUT-5-RI (Pump 220, Reactor Coolant Pump 2-1

Discharge); August 26, 2002

02-05159; Reinspection of Reactor Coolant Pump 2-1 Casing Closure Studs and

Bolting; August 26, 2002

02-05165; LIR - AFW-EQ Overall Assessment; August 27, 2002

02-05262; LIR of Environmental Qualification of SW Pump Room Equipment (IR

02-14-01f); August 29, 2002

02-05296; Containment Analysis Documentation Requirements; August 30, 2002

02-05298; Limiting Containment Temperature May Not Have Been Used in System

Design; August, 30, 2002

02-05300; Ensure That the Containment Spray TSP Baskets are Fully Submerged on

LOCA; August 30, 2002

02-05304; TSP Design Bases; August 30, 2002

02-05322; Additional Review of the Containment is Warranted; August 30, 2002

02-05323; Clarification Required re Containment Vessel Design Pressure;

August 30, 2002

02-05356; Service Water Technical Specification Instruments; September 10, 2002

Attachment

A19

02-05364; LIR - EDG Electrical Capacity C-EE-024.01-005, R8, is to Be Revised;

September 3, 2002

02-05383; LIR EDG-EDG Electrical Capacity C-EE-015.03-002; August 30, 2002

02-05385; LIR - EDG Loading Table Step 1 Block Loading Inadequate; August 30, 2002

02-05390; CR Rollover Exceeds Max Default Times Without Proper Approvals;

September 3, 2002

02-05446; LIR - EDG Loading Could Exceed the EDGs Electrical Capability When

Paralleled; September 4, 2002

02-05459; Split CAC Motor Cables; August 6, 2002

02-05514; System Health Readiness Review (SHRR) Assessment of Testing

Containment Spray Valves - Locked Closed; September 5, 2002

02-05516; LIR - SW Possible Inaccurate Consideration of Design Bases CAC Fouling

Factor; September 5, 2002

02-05559; Inadequate CAP Review of Operating Experience; September 6, 2002

02-05563; Nozzle Flexibility Assumed in Calculations 65A/B is Non-conservative;

September 6, 2002

02-05590; Tornado Missile Protection of Emergency Diesel Generators;

September 6, 2002

02-05593; Thermal Aging Effect of Emergency Core Cooling System Room Post Loss of

Coolant Accident Temperature; September 6, 2002

02-05627; LIR - 59 Percent Undervoltage Relay Logic Shown in EC128AI Is Incorrect;

September 7, 2002

02-05628; LIR - 59 Percent Undervoltage Relay Logic Shown in SD-003A Is Incorrect;

September 7, 2002

02-05632; LIR - Tech Spec Table 3.3-4 Trip Setpoint Tolerance Is Inadequate;

September 7, 2002

02-05633; USAR Discrepancy with LOOP Timing; September 7, 2002

02-05639; Updated Safety Analysis Report Description of Limiting Strainer Size;

September 10, 2002

02-05640; LIR - No Design Bases/Flow Verification Testing of SW Flow to AFW

System; September 10, 2002

Attachment

A20

02-05645; Fuel Assembly NJ10KK Spacer Grid Damage; September 6, 2002

02-05691; LIR - Minimum Temperature to the AFW System SG Nozzles;

September 12, 2002

02-05727; Design Capacity of Ultimate Heat Sink; September 14, 2002

02-05732; License Amendment Request 96-0008 Not Supported by Analysis;

September 10, 2002

02-05738; Relief Valve Set Point Not Conservative; September 11, 2002

02-05748; Lack of Service Water and Ultimate Heat Sink Design Basis for Seismic

Event and Single Active Failure; September 14, 2002

02-05749; LIR - CCW Non-Seismic Piping Over Safety Related Components;

September 12, 2002

02-05784; Service Water Strainer Design Flow; September 11, 2002

02-05848; LIR - EDG High Temperature Evaluation Internal Temperature Rise for

Cabinets; September 12, 2002

02-05870; LIR - EQ List of 10 CFR 50.49 Components; September 12, 2002

02-05881; Reactor Coolant Pump 2-2 Casing Closure Studs and Bolting;

September 12, 2002

02-05885; No Emergency Core Cooling System Air Cooler Inspection Acceptance

Criteria; September 14, 2002

02-05895; Fuel Assembly NJ10LC Spacer Grid Damage; September 13, 2002

02-05896; Fuel Assembly NJ10KL Spacer Grid Damage; September 13, 2002

02-05904; Auxiliary Feedwater Design Basis Calculations Not Located;

September 14, 2002

02-05914; LIR - EDG Lube Oil Procedure Guidance; September 12, 2002

02-05922; LIR - Discrepancy in EDG Voltage and Frequency During Loading;

September 12, 2002

02-05923; No Design Basis for Service Water Pump Net Positive Suction Head

Available; September 16, 2002

02-05925; LIR - EDG Transient Analysis During Loading Sequence - Calculations;

September 12, 2002

Attachment

A21

02-05986; Ultimate Heat Sink Water Inventory Analysis Does Not Consider All Water

Losses; September 14, 2002

02-06062; LIR - EDG: Fuel Filter Inlet Operating Pressure Exceeds Vendor Limits for

Change; September 14, 2002

02-06064; SSDI Item - SW Flow Balance Margins and Need for Additional Recorded

Data; September 14, 2002

02-06100; SSDI Assessment Identified Incorrect Information in OJ 2000-14

(SW Valve Issue); September 14, 2002

02-06108; LIR - AFW Pumps and H2 Dilution Blower Not Evaluated for High Pressure

Injection System; September 14, 2002

02-06134; Service Water Dead Leg Inspection and Cleaning; September 18, 2002

02-06160; Debris Other than Paint Chips Identified in Fuel Assemblies;

September 18, 2002

02-06166; LIR - SW Flow Balance Testing of Alternate Safety Related Return Flow

Paths; September 18, 2002

02-06178; Spacer Grid Damage Observed During Fuel Inspections;

September 18, 2002

02-06215; Excessive Indicated Total RCS Flow Error in SP-03358; September 18, 2002

02-06275; Degraded Makeup Valve MU11 Hardware; September 19, 2002

02-06305; SSDI Item - C-EE-015.03-003, Steady-State Analysis: ELMS;

September 19, 2002

02-06333; Inadequate SW Thermal Analysis; September 19, 2002

02-06337; SSDI Item - SW C-NSA-011.01-007, Revision 1 Concerns (Pump Curves);

September 19, 2002

02-06341; LIR - SW: Review of Industry Experience; September 20, 2002

02-06343; Nuclear Quality Assurance Stop Work on Nuclear Fuel Movements;

September 20, 2002

02-06356; Calculational Process Concerns; September 20, 2002

02-06370; SSDI Item - ECCS Pump Room Heat Load is Non-conservative;

September 20, 2002

Attachment

A22

02-06384; SSDI Item - Enhancement to Calculation 50.20 Flooding of ECCS Rooms

Due to a Feedwater Line Break; September 20, 2002

02-06407; SSDI Item - Instrument Uncertainty in Calibration and Surveillance of

Instrumentation; September 16, 2002

02-06438; Inadequate SW Thermal Analysis; September 2002

02-06439; LIR - SW Service Water Pump Run Out; September 2002

02-06477; SSDI Item - HPI Pump Performance Not Evaluated For Expected Input

Power Variations; September 2002

02-06536; LIR - RCS: PZR Vent Flow Capacity Has No Design Basis; September 2002

02-06547; Design Basis Validation - Pressurizer Vent Orifice Sizing; September 2002

02-06564; Service Water System Cleanliness for Restart; October 5, 2002

02-06677; Ineffective Corrective Action for Locked High Radiation Area Access Control;

September 25, 2002

02-06701; Post-LOCA Dose from BWST with Inadvertent HP31/HP32 Failure;

September 25, 2002

02-06702; Potential for Inadequate HPI Pump Minimum Recirculation Following LOCA;

September 25, 2002

02-06723; LIR - NRC Concern Regarding Sites Lubrication Program;

September 26, 2002

02-06725; Sway Strut Bushing Grease Fittings; September 26, 2002

02-06737; SSDI Item - C-EE-004.01-051 Uncertainty Treatment; September 25, 2002

02-06757; LIR - EDG Potential Overload Condition; September 26, 2002

02-06767; LIR - AFW (JCO) Inputs Not Bounding; September 26, 2002

02-06773; LIR - AFW CR 95-0906 Deficiencies; September 26, 2002

02-06779; Voltage Reading Exceeded Tolerance and Evidence of Heat Damage;

September 26, 2002

02-06821; LIR - AFW Pump Surveillance Testing; September 26, 2002

02-06860; Review of the Need for Relief Valves for Several Heat Exchangers;

September 27, 2002

Attachment

A23

02-06861; Bearing Oil Cooler Strainer Fouling; September 27, 2002

02-06885; Reactor Coolant System Flow Uncertainty May Be Higher than Assumed;

September 27, 2002

02-06893; Effect of Room 105, and 115 Temp Increase; September 24, 2002

02-06951; LIR - EDG Engine Derating; September 27, 2002

02-06986; Relay Testing; September 26, 2002

02-06996; HPI Flow Test Acceptance Criteria Versus T.S. 4.5.2.H; September 27, 2002

02-07110; Unqualified Splice in MOV; October 1, 2002

02-07148; LIR CCW - Lack Of Functional Testing Of Letdown Cooler And RCP

Interlocks; October 1, 2002

02-07153; LIR - EDG Appendix R Load Calculation; October 1, 2002

02-07159; Lack of Valve Position Alarm; October 1, 2002

02-07188; Non-conservative Assumptions in 67.005, Service Water Ventilation

Capacity; October 1, 2002

02-07236; LIR - AFW SG Accident Pressure versus AFW Pump Flow; October 1, 2002

02-07278; RC2 Pressurizer Spray Valve Design; October 1, 2002

02-07328; Lack of Timeliness for Radiation Protection Action Implementation;

October 3, 2002

02-07378; LIR - SW to CCW Makeup Line Flow Verification Test Discrepancies;

October 3, 2002

02-07402; Reactor Coolant Pump Vendor Technical Manual Closure Stud Elongation

Specification Should be Updated; October 3, 2002

02-07468; Inappropriate SW Pump Curve Allowable Degradation; October 3, 2002

02-07475; Instrument Inaccuracy for Air Temperature Not Considered in SW Vent

Calculations; October 3, 2002

02-07516; LIR - CAC SW Flow Tests Indicate Adverse Trend; September 9, 2002

02-07524; LIR - AFW Pump Curves; October 2002

02-07559; LIR - RCS: Lack of Response to Request For Assistance for Design Basis

Validation Information; October 2002

Attachment

A24

02-07596; EDG High Temperature Overall; October 17, 2002

02-07599; LIR - EDG High Temperature - Determine Capability to Function;

October 2002

02-07600; LIR - RCS Inappropriate Cancellation of Mod 90-0012; October 7, 2002

02-07609; Cable Separation of Hi Point Valves; October 7, 2003

02-07640; No Overpressure Protection Evaluation for Isolable Components;

October 8, 2002

02-07646; SSDI Item - Calc C-EE-004.01-051 Temperature Variation Not Considered

October 8, 2002

02-07657; Service Water Pump Design Flow Rate in Question; October 8, 2002

02-07684; HPI Pump Operation Under Long Term Minimum Flow; October 8, 2002

02-07692; USAR Section 9.2.5.1 Concerning Placing SW Pumps into Operation After

13 Hours; October 8, 2002

02-07701; Control Room Operator Dose Due to ECCS Leakage Post-LOCA;

October 9, 2002

02-07706; Multiple Open Work Orders to Install Inspection Opening in Service

Structure; October 9, 2002

02-07713; Post Accident Control Room Dose Calculations; October 9, 2002

02-07714; Inadequate Flooding Protection for the SW Pump House; October 9, 2002

02-07716; Wrong Instrument May Be Used to Verify Ultimate Heat Sink Temperature;

October 9, 2002

02-07750; Lack of a Design Basis Analysis for Containment Isolation Valve Backup Air

Supplies (IR 02-14-01a); October 9, 2002

02-07757; Environmental Conditions for Decay Heat Pump Seal Leak Not Evaluated;

October 9, 2002

02-07760; Flood Analysis Discrepancies in the Service Water Pipe Tunnel and Valve

Rooms; October 9, 2002

02-07766; Non-conservative Value for 90 Percent Volt in Table 3.3-4; October 9, 2002

02-07781; Weaknesses in Testing Service Water Outlet Valves to Containment Air

Coolers; October 9, 2002

Attachment

A25

02-07802; Basis for PSH 2929 and PSH 2930 Not Found; October 10, 2002

02-07889; Open Item for Screen Wash and Service Water Systems; October 11, 2002

02-07981; Intake Gantry Crane; October 14, 2002

02-07986; HGA Relay Failures; October 14, 2002

02-08010; GE SBM Switch Failures; October 14, 2002

02-08183; Differential Pressure Switch Error; October 16, 2002

02-08251; Concerns with Ultimate Heat Sink Analysis Post Loss of Coolant Accident;

October 17, 2002

02-08278; Maximum Allowable Pressurizer Level Should be 228 inches, Not 305 inches;

October 17, 2002

02-08281; Additional Errors in SW Ventilation Calculation 67.005; October 17, 2002

02-08331; System Improvement: AFW - Clarify SSE+ LOCA Licensing Basis;

October 20, 2002

02-08482; EDG Rating and Capacity; October 22, 2002

02-08759; Potential Overstress Condition in Reactor Coolant Pump Casing Joint;

October 28, 2002

02-09027; Unqualified Splice in MOV; November 4, 2002

02-09036; Greasing of Struts; November 5, 2002

02-09314; Untimely Determination of Condition Reportability; November 13, 2002

02-09405; SHRR Containment Air Cooler Review; November 2002

02-09737; Reactor Coolant Pump 1-1 Shaft Assembly Has Linear Indications on Upper

and Lower Faces of Journal Support Hub; November 29, 2002

02-09739; 2-2 HPI Thermal Sleeve Degradation; November 29, 2002

02-09829; Damaged Fuel Assembly NJ126J; December 12, 2002

02-09870; EN-DP-01501, RCP22OUTI-1, Reactor Coolant Pump 2-2 and Outlet Pipe;

December 5, 2002

02-09928; HPI Thermal Sleeve 2-1 Degradation; December 2002

02-09947; Inadequate Tracking of Condition Report Rollovers; December 14, 2002

Attachment

A26

02-10369; Condition Report Trend Analysis Not Performed Regularly;

December 19, 2002

02-10425; 15 Ton Capacity Hoist Trolley on the Gantry Crane; December 20, 2002

03-00120; CAC Thermal Performance Roll-up; January 2003

03-00131; RCS DB-OP-2003 Procedure Enhancements for RCS Leakage Identification;

January 9, 2003

03-00418; Foreign Material Discovery in 2 CAC SW Piping; January 11, 2003

03-00473; Boric Acid Corrosion Control Program - Mode 3 Walkdowns;

January 15, 2003

03-00496; Minor Discrepancies; January 21, 2003

03-00501; Lack of Documentation Confirming Pump DHR/LPI P42-1 Will Not Runout

During Recirculation Phase Operation; January 21, 2003

03-00519; Incorrect Allowable Value Indicated in Conclusion of C-ICE-083.03-004

Revision 2; January 21, 2003 and January 23, 2003

03-00561; MSLB Analysis Credits MSIV Closure Under Reverse Flow; January 23, 2003

03-00563; MSIVs MS100 and MS101 Surveillance Testing/Flowserve Vendor

Documentation; January 23, 2003

03-00568; Bases for Main Steam Safety Valve Relief Capacity Listed in Technical

Specifications Could Not Be Located; January 23, 2003

03-00575; Incorrect Statement in Breaker Setting Calculations; January 2003

03-00770; Three Rollover Errors; January 2003

03-00937; Concern Regarding Intra System Leakage; February 3, 2003

03-00938; Concern Regarding Reactor Coolant Pump Motor 2-2 Oil Lift System;

February 3, 2003

03-00940; Concern Regarding Reactor Coolant Pump Motor Maintenance Program;

February 3, 2003

03-01022; Two Rollover Issues; February 2003

03-01448; EDG Tech Spec Table 3.3-4 Trip Setpoint May Have Been Exceeded;

February 21, 2003

03-01492; Fuel Assembly NJ1271 Damaged Spacer Grid; February 24, 2003

Attachment

A27

03-01648; Unacceptable SG Tube Stresses in Appendix R Cooldown;

February 28, 2003

03-01870; PR/BACC: CR/CA; March 8, 2003

03-01955; CR Rollover Discrepancies; March 12, 2003

03-02220; Emergency Diesel Generator Component Cooling Water Flows Inconsistent

with Modification 97-0029 Requirements; March 20, 2003

03-02699; DB-OP-02519 Does Not Match Plant Configuration; April 4, 2003

03-05925; Weaknesses in Conduct of Trending; July 23, 2003

03-06296; Boric Acid Identified on Reactor Coolant Pump 2-2; August 5, 2003

03-06655; Superceded Calculations Were Not Tracked According to EN-DP-0140;

August 18, 2003

03-07656; Forward Flow Rate of 10,000 Gpm Not Attained for SW19 During

DB-PB-03232; September 12, 2003

03-08196; Mode 3A System Leakage Test; RCP 2-1 Boric Acid Deposits;

September 26, 2003

03-08249, Classification of CR 02-05590 for LER 2002-006 on Tornado Missile

Protection; September 28, 2003

Drawings

E-1037P; Electrical Grounding Details; Sheet 2; Revision 1

E-1037P; Electrical Grounding Details; Sheet 3; Revision 1

E-1037P; Electrical Grounding Details; Sheet 10; Revision 0

E-1037P; Electrical Grounding Details; Sheet 11; Revision 0

E-1042; Emergency Diesel Generator 1-1 Loading Table; Sheet 1; Revision14

E-1042; Emergency Diesel Generator 1-1 Loading Table; Sheet 2; Revision16

E-1043; Emergency Diesel Generator 1-2 Loading Table; Sheet 1; Revision 1 4

E-1043; Emergency Diesel Generator 1-2 Loading Table; Sheet 2; Revision 15

M-006D; Auxiliary Feedwater System; Revision 47

M-017A; Diesel Generators; Revision 1

Attachment

A28

M-017C; Diesel Generators Fuel Oil; Revision 22

M-033A; High Pressure Injection; Revision 30

M-036A; Component Cooling Water System; Revision 24

M-036B; Component Cooling Water System; Revision 30

M-036C; Component Cooling Water System; Revision 25

M-041A; Service Water Pumps and Secondary Service Water System; Revision 25

M-041B; Primary Service Water System; Revision 54

M-041C; Service Water System for Containment Air Coolers; Revision 25

M-096D; Auxiliary Feedwater System; Revision 47

7749-M-508-74-8; Byron-Jackson Reactor Coolant Pump; Sheets 1 and 2; Revision D

7M-017B; Diesel Generators Air Start; Revision 32

Engineering Change Packages and Requests

99-0039-00; Replacement of Containment Air Cooler Service Water Discharge Valves;

Revision 1

01-0306A; At Risk Change: Component Cooling Water Heat Exchanger Bolt

Replacement and Deletion of Relief Valves SW3962 and SW3963; April 18, 2003

01-0306B; At Risk Change: Component Cooling Water Heat Exchanger Bolt

Replacement and Deletion of Relief Valves SW3962 and SW3963; April 22, 2003

03-0074-00; Install Larger Mesh in Strainer Baskets on Service Water Inlet to Auxiliary

Feedwater Pumps and New Strainers Upstream of the Restricting Orifices;

June 19, 2003

03-0243-00; Rewire the Control Circuitry for CAC Fan 1-1 Such That in the Case of a

Control Room Fire, This Fan Can Be Started in Slow Speed to Provide Cooling to the

Containment; July 2003

03-0267-00; Provide Level and Pressure Indication for the Idle SG on the Auxiliary

Shutdown Panel to Support Appendix R Safe Shutdown; July 2003

Engineering Work Requests

01-0306-00; Remove Service Water Header Relief Valves; December 10, 2001

Attachment

A29

01-0378-00; Provide Larger Access Holes to Enable Removal of Boric Acid;

August 30, 2001

02-0138-00; RV Service Structure Support Skirt Openings; April 11, 2002

02-0217-00; Replace Existing Reactor Vessel Head; June 4, 2002

Evaluations

Basic Cause Analysis Report for CR 02-09314

Root Cause Analysis for CR 03-00425

Root Cause Analysis for CR 02-04673; March 18, 2003

Root Cause Analysis for CR 02-06178; February 1, 2003

Root Cause Analysis for CR 03-02597

Operability Evaluation 02-0036; Tornado Missile Protection Issues; December 17, 2002

Operability Evaluation 03-0009; Revision 1 for CR 03-00949

Information Notices

80-13; General Electric Type SBM Control Switches - Defective Cam Follower;

April 4, 1980

85-94; Potential for Loss of Minimum Flow Paths Leading to ECCS Pump Damage

During a LOCA; December 13, 1985

97-12; Potential Armature Binding in General Electric Type HGA Relays;

March 24, 1977

98-19; Shaft Binding in General Electric Type SBM Control Switches; June 3, 1978

Inspection Manual Chapters

0305; Operating Reactor Assessment Program; February 19, 2003

0350; Oversight of Operating Reactor Facilities in an Extended Shutdown as a Result of

Significant Performance Problems; March 6, 2001

0609; Significance Determination Process; April 21, 2003

Appendix A; Significance Determination of Reactor Inspection Findings for

At-Power Situations; March 18, 2002

Attachment

A30

Appendix C; Occupational Radiation Safety Significance Determination Process;

June 24, 2003

Appendix D; Public Radiation Safety Significance Determination Process; July

24, 2003

Appendix F; Fire Protection Significance Determination Process;

February 27, 2001

Appendix H (Draft) Containment Integrity Significance Determination Process;

July 8, 2003

0612; Power Reactor Inspection Reports; June 20, 2003

Inspection Reports

05000346/1995007; Routine Inspection Report; September 29, 1995

05000346/1999001; Routine Inspection Report; March 5, 1999

05000346/1999004; Routine Inspection Report; June 7, 1999

05000346/2002003; Augmented Inspection Team - Degradation of the Reactor

Pressure Vessel Head; May 3, 2002

05000346/2002012; Special Inspection - Boric Acid Corrosion Extent of Condition;

November 29, 2002

05000346/2002014; Safety System Design and Performance Capability Inspection;

February 26, 2003

05000346/2002017; Integrated Inspection Report; December 9, 2002

05000346/2002019; Integrated Inspection Report; January 31, 2003

Intra-Company Memoranda

NPE 01-00071; OE 12074 - Boric Acid Corrosion of Carbon Steel Components at the

Reactor Coolant System Pressure Boundary; April 27, 2001

NPE 02-00227; Reactor Coolant Pump Issues; August 9, 2002

NPE 03-00047; Reactor Coolant Pump Status to August 9, 2002, White Paper;

April 3, 2003

Generic Letters 89-13; Service Water System Problems Affecting Safety-Related Equipment;

July 18, 1989 and Supplement 1; April 4, 1990

Attachment

A31

91-18; Information to Licensees Regarding Two NRC Inspection Manual Sections on

Resolution of Degraded and Non-Conforming Conditions and on Operability; Revision 1,

October 8, 1997

96-06; Assurance of Equipment Operability And Containment Integrity During

Design-Basis Accident Conditions; September 30, 1996 and Supplement 1; November

13, 1997

Letters

Amendment 33 to Facility Operating License NPF-3 for Davis-Besse Nuclear Power

Station Unit No.1, NRC to Toledo Edison; October 1, 1980

Amendment 45 to Facility Operating License NPF-3 Cycle 3 Operation, NRC to Toledo

Edison; July 28, 1982

Amendment 80 to Facility Operating License NPF-3 Cycle 5 Operation, NRC to Toledo

Edison; December 13, 1984

Component Cooling Water System, First Energy S/N 2949; May 21, 2003

Davis-Besse Nuclear Power Station, Unit 1 - Requests For Relief for the Third 10-year

Interval Inservice Inspection Program Plan (TAC MB1607), NRC to First Energy;

September 30, 2002

Davis-Besse Reactor Coolant Pump Casing Joint Analysis, Flowserve to First Energy;

April 24, 2003

Davis-Besse Reactor Coolant Pump Shaft Bearing Cracking, MPR Associates to First

Energy; February 7, 2003

Evaluation of Ultimate Heat Sink Pond Thermal Performance, Bechtel to First Energy;

May 19, 2002

Exemption from Certain Requirements of Appendix R to 10 CFR Part 50, NRC to Toledo

Edison; August 23, 1984

Inspection of Davis-Besse Reactor Coolant Pumps 2-1 and 2-2, Flowserve to First

Energy; September 16, 2002

Issuance of Amendment 11 to Facility Operating License NPF-3 for Davis-Besse

Nuclear Power Station Unit 1, NRC to Toledo Edison; June 16, 1978

Reactor Coolant Pump Inter-Gasket Leakoff, Flowserve to First Energy; July 2, 2002

Return to Service of Davis-Besse Reactor Coolant Pumps 2-1 and 2-2, Flowserve to

First Energy; February 4, 2003

Attachment

A32

Licensee Event Reports (LERs)

LER 2002-006; EDG Exhaust Piping Not Adequately Protected From Potential Tornado-

Generated Missiles; November 5, 2002

LER-2002-008; Review and Evaluate Containment Air Coolers Collective Significance

LER; Revisions 0 and 1

LER-2002-009; Degradation of High Pressure Injection Thermal Sleeves;

February 3, 2002

LER 2003-007; AC System Analysis Shows Potential Loss of Off-Site Power Following

Design Basis Event; August 5, 2003

Maintenance Work Orders

1-87-3304-00; Check Stud Elongation on All Four Reactor Coolant Pumps;

July 21, 1988

1-97-0553-00; Check P36-1 Casing Studs; May 14, 1998

1-97-0553-01; Check P36-2 Casing Studs; May 14, 1998

1-97-0553-02; Check P36-3 Casing Studs; May 14, 1998

1-97-0553-03; Check P36-4 Casing Studs; May 14, 1998

1-97-0817-04; Reactor Coolant Pump Motor 2-2; April 15, 1998

7-96-0650-01, -02, and -05; Enclosure 7 of DB-MM-09117, R0, Tensioning Data Sheet

from Work Orders for Reactor Coolant Pumps 1-1, 1-2, and 2-1, Respectively

7-96-0650-06; Work in Progress Log, Reactor Coolant Pump 2-2

02-002724-000; Replace Upper Shaft Labyrinth Seal on Reactor Coolant Pump 2-2;

May 6, 2002

02-007012-000; Service Water Pumps and Piping; March 7, 2003

02-007451-000; Temperature Indicator at Service Water Header 1; March 5, 2003

Miscellaneous Documents

Basic Cause Categories Chart; February 27, 1996

Component Parameter Scoping Sheet for Reactor Coolant Pump Vibration Monitoring

1012; Revision 3

CNRB Loss Prevention Subcommittee Meeting; April 23, 2003

Attachment

A33

Condition Report Trending Presentation; August 13, 2003

Corrective Action Program Performance Indicators; various dates

CR Summary Report for Managers Meeting Discussion; August 13, 2003

Davis-Besse EAB August 2003 Monthly Meeting; August 26, 2003

Davis-Besse AC Electrical Distribution Systems, Summary of Issues and Approach for

Resolution; May 15, 2003

Davis-Besse Self Evaluation Process Guide; April 25, 2001

EPRI Topical Report NP-2005; Tornado Missile Risk Evaluation Methodology, Volumes I

and II; August 1981

License Amendment Request 96-0008;Increasing Ultimate Heat Sink Temperature;

July 28, 1999

License Amendment Request 03-0002; to Revise TS 3/4.5.2 ECCS Subsystems - Tavg

> 280F; Revision 25

Managers Communication and Teamwork Meeting; August 26 and 28, 2003

NEI 96-07; Guidelines for 10 CFR 50.59 Implementation; Revision 1

NRC SER; EPRI Topical Reports Concerning Tornado Missile Probabilistic Risk

Assessment (PRA) Methodology; 1983

Photographs Showing Results of Non-Destructive Testing of the 1-1 Pump Shaft Journal

Support Hub; January 14, 2003

Plant Engineering Policy PE-17 Trending; Revision 1

Pre-fire Plans for Rooms AB-318 and AB-319

PR-IAP-3A-01; CAP Implementation Issues Resolution and Restart Readiness;

Revision 2

Quality Trend Summary, First Quarter 2002 Condition Reports; June 3, 2002

Request for Modification 94-0025; Install Service Structure Inspection Openings; Voided

August 31, 1999

Resolution of System Health Assurance Plan Design Issues; December 18, 2002

Restart Performance Indicators; August 3, 2003

Taproot Root Cause Tree Chart; February 27, 1996

Attachment

A34

Technical Specification Table 3.3-4

Three Day CA Look Ahead; March, 19, 2003

Time Line for Reactor Coolant Pump Casing Stud Tension Evaluation; August 15,2003

USAR Change 02-063; Revise Safety Analysis Report to Reflect Use of TORMIS;

November 22, 2002

USAR Chapter 8; Electrical

USAR Figure 9.3-16; Functional Drawing Makeup and Purification System; Revision 20

NQA Audits and Self Assessment Reports

DB-C-02-02; NQA Assessment Report; August 9, 2002

DB-C-02-03; NQA Assessment Report; November 14, 2002

DB-C-02-04; NQA Assessment Report; February 19, 2003

DB-C-03-01; NQA Assessment Report; May 28, 2003

DB-C-03-02; NQA Assessment Report; September 1, 2003

DB-C-03-03; NQA Assessment Report; November 17, 2003

2002-0085; Self Assessment Report, Operating Experience Program; October 3, 2002

Self Evaluation Report; June 2002

Self Assessment Report, Electrical Transient Analysis Program (ETAP) June 2-6, 2003;

Revision 1

NUREGs

0800; Standard Review Plan for the Review of Safety Analysis Reports for Nuclear

Power Plants; Revision 1

1649; Reactor Oversight Process; Revision 3; July 2000

CR 6762; GSI-191 Technical Assessment: Parametric Evaluations for Pressurized

Water Reactor Recirculation Sump Performance; August 2002

Potential Condition Adverse to Quality Reports

1991-0173; ECCS Room Cooling Units; May 14, 1991

1993-0256; Potential Condition Adverse to Quality Report; April 19, 1993

Attachment

A35

1998-0126; Post Accident Sampling Pump P-218 Has Seal Design Which Is Not Leak

Tight; January 25, 1998

Procedures

Self Evaluation Process Guidelines; April 25, 2001

DBBP-LP-2000; Condition Report Process Implementation Expectations; April 4, 2003

DBBP-PI-2005; Cause Analysis Review Group; February 7, 2003

DB-ME-03002; Station Battery Service and Performance Discharge Test; Revision 4

DB-ME-09500; Installation and Termination of Electrical Cables

DB-MM-09320; Jacket Water Heat Exchanger Maintenance; Revision 5

DB-OP-01200; Reactor Coolant System Leakage Management; Revision 5

DB-OP-02037; Emergency Diesel Generator Alarm Panel 37 Operating Procedure;

Revision 2

DB-OP-06016; Containment Air Cooler System Operating Procedure; Revision 2

DB-OP-06261; Service Water System Operating Procedure; Revision 2

DB-OP-06406; Steam and Feedwater Rupture Control System Operation Procedure;

Revision 4

DB-PF-03008; Containment Local Leakage Rate Tests; Revision 5

DB-PF-03020; Service Water Train 1 Valve Test; Revision 5

DB-PF-03027; Service Water Train 2 Valve Test; Revision 5

DB-PF-03117; Baseline and Comprehensive Testing of Service Water Pump 1;

Revision 3

DB-PF-03123; Baseline and Comprehensive Testing of Service Water Pump 2;

Revision 5

DB-PF-03130; Baseline and Comprehensive Testing of Service Water Pump 3;

Revision 5

DB-PF-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed

Trip Test; Revision 5

DB-SC-03023; Off-site AC Sources Lined Up and Available; Revision 6

Attachment

A36

DB-SP-03000; Service Water Integrated Train I Flow Balance Procedure

DB-SP-03001; Service Water Integrated Train II Flow Balance Procedure

DB-SP-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed

Trip Test

EN-DP-01080; Calculations; Revision 0

NG-EN-00327; RCS Integrated Leakage Program; Revision 0

NG-EN-00385; Program Compliance Review; Revision 0

NG-NA-00711; Quality Trending; March 1, 2003

NG-VP-00100; Restart Action Plan Process; February 6, 2003

NOBP-LP-2007; Condition Report Process Effectiveness Review; March 1, 2003

NOBP-LP-2001; FENOC Focus Self Assessment Guideline; Revisions 0 and 1

NOBP-LP-2004; FENOC Ongoing Self Assessment Guideline; Revision 0

NOBP-LP-2008; Corrective Action Review Board; Revision 0

NOBP-LP-2010; Crest Trending Codes; Revision 0

NOP-CC-3002; Nuclear Operating Administrative Procedure; Revision 0

NOP-ER-1001; Continuous Equipment Performance Improvement; Revision 1

NOP-ER-3001; Problem Solving and Decision Making Process; Revision 0

NOP-LP-2001; Condition Report Process; Revisions 3 and 4

NOP-LP-2004; Internal Assessment Process; Revision 1

RA-EP-02830; Emergency Plan Off Normal Occurrence Procedure; Revision 1

Regulatory Guides

1.4; Assumptions Used for Evaluating the Potential Radiological Consequences of a

Loss of Coolant Accident for Pressurized Water Reactors; Revision 2

1.187; Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and

Experiments; November 2000.

Attachment

A37

Reports

Corrective Action Program Review Summary Report; September 2002

Collective Significance Report Containment Air Cooler Thermal Performance;

March 21, 2003

Assessment of Thermal Performance for the Containment Air Coolers; April 22, 2003

Assessment of Thermal Performance for the Containment Air Coolers; August 9, 2003

Emergency Diesel Generator 1 Jacket Water Cooler Eddy Current Test Report;

July 31, 2002

Emergency Diesel Generator 2 Jacket Water Cooler Eddy Current Test Report;

July 9, 2003

Operating Experience Report 15262; Byron Jackson Reactor Coolant Pump

Casing-to-cover Leakage; January 23, 2003

Operating Experience Report 15383; Preliminary Linear Indications on the Reactor

Coolant Pump 1-1 Shaft Assembly; January 21, 2003

Surveillances

DB-ME-03002; Battery Service Test; completed March 2002

DB-PF-03065; Pressure and Augmented Leakage Test; completed April 2, 2000,

August 27, 2002, and August 28, 2002

DB-PF-04152; Auxiliary Feedwater Pump Turbine 1 High Speed Stop and Overspeed

Trip Test; completed May 10, 2002

DB-SP-03357; Reactor Coolant System Water Inventory Balance; completed

May 3, 1993, November 21, 1994, May 29, 1996, May 23, 1998, and May 22, 2000

DB-SP-03358; Reactor Coolant System Flow Rate Test; completed August 25, 2000

DB-SP-04360; Reactor Coolant System Flow Test; completed August 11, 2000

DB-SP-04363; Reactor Coolant Pumps Hand Rotation; completed August 19, 2003,

September 23, 2003, and October 23, 2003

10 CFR 50.59 Applicability Determination, Screen and Evaluations

02-01740; TORMIS Methodology for Tornado Missile Risk Evaluation;

November 13, 2002

Attachment

A38

03-00087; Screen Use of Fuel Assemblies with Spacer Grid Damage in the Cycle 14

Core - Modes 3, 4, 5, 6; February 1, 2003

Vendor Manual

03-5001383-01; Reactor Coolant Pump Motor Bearing Maintenance, Pages 89AA

through 105; completed April 17 through May 6, 1998

M-001-1; Westinghouse Product Update: Recommended 1-Year, 5-Year, and 10-Year

Reactor Coolant Pump Motor Inspection and Maintenance; November 1991

Attachment

A39

LIST OF ACRONYMS USED

AC

Alternating Current

ADAMS

Agency-wide Document Access and Management System

AIT

Augmented Inspection Team

AFW

Auxiliary Feedwater

ASME

American Society of Mechanical Engineers

AV

Apparent Violation

BACC

Boric Acid Corrosion Control

BWST

Borated Water Storage Tank

B&W

Babcock and Wilcox

CAC

Containment Air Cooler

CARB

Corrective Action Review Board

CAP

Corrective Action Program

CATI

Corrective Action Team Inspection

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CR

Condition Report

CRDM

Control Rod Drive Mechanism

CS

Containment Spray

DC

Direct Current

DHR

Decay Heat Removal

EAB

Engineering Assessment Board

ECCS

Emergency Core Cooling System

ECR

Engineering Change Request

EDG

Emergency Diesel Generator

EPRI

Electric Power Research Institute

EQ

Environmental Qualification

ESF

Engineered Safety Feature

ETAP

Electric Transient Analysis Profile

FENOC

FirstEnergy Nuclear Operating Company

FIN

Finding

GDC

General Design Criteria

GL

Generic Letter

GPM

Gallons per Minute

HPI

High Pressure Injection

HPR

High Pressure Recirculation

IMC

Inspection Manual Chapter

IN

Information Notice

IR

Inspection Report

ISI

In-service Inspection

IST

In-service Testing

KSI

Kilo (1000) Pounds per Square Inch

kV

Kilo Volt (1000 volts)

LAR

License Amendment Request

lb/ft3

Pounds per Cubic Foot

LER

Licensee Event Report

LIR

Latent Issues Review

LOCA

Loss of Coolant Accident

Attachment

A40

LIST OF ACRONYMS USED, contd.

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

MRB

Management Review Board

MSSV

Main Steam Safety Valve

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NOBP

Nuclear Operations Business Practice

NOP/NOT

Normal Operating Pressure and Normal Operating Temperature

NPSH

Net Positive Suction Head

NQA

Nuclear Quality Assessment

NRC

United States Nuclear Regulatory Commission

NRR

Office of Nuclear Reactor Regulation

OI

Office of Investigations

PARS

Publicly Available Records

PI

Performance Indicator

PORV

Power Operated Relief Valve

PRA

Probabilistic Risk Assessment

PRC

Project Review Committee

PSIG

Pounds Per Square Inch Gauge

RCPB

Reactor Coolant Pressure Boundary

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RFO

Refueling Outage

RSRB

Restart Station Review Board

SCAQ

Significant Condition Adverse to Quality

SDP

Significance Determination Process

SG

Steam Generator

SHA

System Health Assurance

SRA

Senior Reactor Analyst

SRB

Station Review Board

SSC

Structures, Systems, Components

SSDI

Safety System Design and Performance Capability Inspection

SW

Service Water

the Code

ASME Boiler and Nuclear Pressure Vessel Code

TPCS

Transient without Power Conversion System

TS

Technical Specifications

TSP

Tri-Sodium Phosphate

UHS

Ultimate Heat Sink

URI

Unresolved Item

USAR

Updated Safety Analysis Report

V

Volts

Vac

Volts (alternating current)

Vdc

Volts (direct current)

VIO

Violation

WO

Work Order

F

Degrees Fahrenheit