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| issue date = 11/09/2007
| issue date = 11/09/2007
| title = IR 05000247-07-004, on 07/01/2007 - 09/30/2007; Indian Point, Unit 2; Fire Protection, Maintenance Risk Assessment and Emergent Work Control, and Surveillance Testing
| title = IR 05000247-07-004, on 07/01/2007 - 09/30/2007; Indian Point, Unit 2; Fire Protection, Maintenance Risk Assessment and Emergent Work Control, and Surveillance Testing
| author name = Cobey E W
| author name = Cobey E
| author affiliation = NRC/RGN-I/DRP/PB2
| author affiliation = NRC/RGN-I/DRP/PB2
| addressee name = Dacimo F R
| addressee name = Dacimo F
| addressee affiliation = Entergy Nuclear Operations, Inc
| addressee affiliation = Entergy Nuclear Operations, Inc
| docket = 05000247
| docket = 05000247
Line 19: Line 19:


=Text=
=Text=
{{#Wiki_filter:UNITED STATES  NUCLEAR REGULATORY COMMISSION    REGION I    475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406 November 9, 2007  
{{#Wiki_filter:November 9, 2007


Mr. Fred Site Vice President Entergy Nuclear Operations, Inc.
==SUBJECT:==
 
INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED INSPECTION REPORT 05000247/2007004
Indian Point Energy Center 450 Broadway, GSB P.O. Box 249 Buchanan, NY 10511-0249
 
SUBJECT: INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED INSPECTION REPORT 05000247/2007004


==Dear Mr. Dacimo:==
==Dear Mr. Dacimo:==
On September 30, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report documents the inspection results, which were discussed on October 3, 2007, with Mr. Anthony Vitale and other members of your staff.
On September 30, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report documents the inspection results, which were discussed on October 3, 2007, with Mr. Anthony Vitale and other members of your staff.


The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


This report documents three findings of very low safety significance (Green). These findings were also determined to be violations of NRC requirements. However, because of their very low safety significance, and because they were entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCV's) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a written response within 30 days of the date of this inspection report with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington D.C. 220555-001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 2.
This report documents three findings of very low safety significance (Green). These findings were also determined to be violations of NRC requirements. However, because of their very low safety significance, and because they were entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a written response within 30 days of the date of this inspection report with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington D.C. 220555-001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 2.


In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/ Eugene W. Cobey, Chief Projects Branch 2 Division of Reactor Projects  
Sincerely,
/RA/  
 
Eugene W. Cobey, Chief Projects Branch 2 Division of Reactor Projects  


Docket No. 50-247 License No. DPR-26  
Docket No. 50-247 License No. DPR-26  


===Enclosure:===
Enclosure: Inspection Report No. 05000247/2007004  
Inspection Report No. 05000247/2007004 w/


===Attachment:===
w/ Attachment: Supplemental Information  
Supplemental Information  


cc w/encl: J. Wayne Leonard, Chairman and CEO, Entergy Nuclear Operations, Inc.
cc w/encl:
J. Wayne Leonard, Chairman and CEO, Entergy Nuclear Operations, Inc.


G. J. Taylor, Chief Executive Officer, Entergy Operations M. Kansler, President & CEO/CNO, Entergy Nuclear Operations, Inc.
G. J. Taylor, Chief Executive Officer, Entergy Operations M. Kansler, President & CEO/CNO, Entergy Nuclear Operations, Inc.
Line 57: Line 56:
J. Lynch, Manager, Licensing (ENO)
J. Lynch, Manager, Licensing (ENO)
E. Harkness Director of Oversight (ENO)
E. Harkness Director of Oversight (ENO)
P. Conroy, Director, Nuclear Safety Assurance W. Dennis, Assistant General Counsel, Entergy Nuclear Operations, Inc. P. Tanko, President and CEO, New York State Energy Research and Development Authority P. Eddy, Electric Division, New York State Department of Public Service P. Smith, President, NYS Energy, Research, and Development Authority C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law D. O'Neill, Mayor, Village of Buchanan J. G. Testa, Mayor, City of Peekskill R. Albanese, Four County Coordinator S. Lousteau, Treasury Department, Entergy Services, Inc.
P. Conroy, Director, Nuclear Safety Assurance W. Dennis, Assistant General Counsel, Entergy Nuclear Operations, Inc.
 
P. Tanko, President and CEO, New York State Energy Research and Development Authority P. Eddy, Electric Division, New York State Department of Public Service P. Smith, President, NYS Energy, Research, and Development Authority C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law D. ONeill, Mayor, Village of Buchanan J. G. Testa, Mayor, City of Peekskill R. Albanese, Four County Coordinator S. Lousteau, Treasury Department, Entergy Services, Inc.


Chairman, Standing Committee on Energy, NYS Assembly Chairman, Standing Committee on Environmental Conservation, NYS Assembly Chairman, Committee on Corporations, Authorities, and Commissions M. Slobodien, Director, Emergency Planning W. Dennis, Assistant General Counsel
Chairman, Standing Committee on Energy, NYS Assembly Chairman, Standing Committee on Environmental Conservation, NYS Assembly Chairman, Committee on Corporations, Authorities, and Commissions M. Slobodien, Director, Emergency Planning W. Dennis, Assistant General Counsel
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The report covered a three-month period of inspection by resident and region-based inspectors.
The report covered a three-month period of inspection by resident and region-based inspectors.


Three findings of very low significance were identified. These findings were determined to be non-cited violations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, "Significance Determination Process."
Three findings of very low significance were identified. These findings were determined to be non-cited violations. The significance of most findings is indicated by their color (Green, White,
Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process.


Findings for which the significance determination process (SDP) does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
Findings for which the significance determination process (SDP) does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
 
===A. NRC-Identified and Self-Revealing Findings===


===NRC-Identified and Self-Revealing Findings===
===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
The inspectors identified a non-cited violation (NCV) of License Condition 2.K., fire protection program, because Entergy failed to identify a degraded three-hour rated fire door on the east entrance of the 12 fire main booster pump room. The door was determined to be inoperable due to a misalignment, which prevented the door from fully closing. Entergy entered this issue into their corrective action program, took immediate compensatory actions, realigned the door, and ensured that it would fully close.
The inspectors identified a non-cited violation (NCV) of License Condition 2.K., fire protection program, because Entergy failed to identify a degraded three-hour rated fire door on the east entrance of the 12 fire main booster pump room. The door was determined to be inoperable due to a misalignment, which prevented the door from fully closing. Entergy entered this issue into their corrective action program, took immediate compensatory actions, realigned the door, and ensured that it would fully close.


The inspectors determined that this finding was more than minor because it was associated with the protection against external factors attribute of the Mitigating Systems cornerstone; and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding was evaluated using Phase 1 of Inspection Manual Chapter (IMC) 0609 Appendix F, "Fire Protection Significance Determination Process.The inspectors determined that this issue was of very low safety significance because the degradation of the fire barrier was "moderate" based on the fire door displaying significant degradation affecting its performance or reliability.
The inspectors determined that this finding was more than minor because it was associated with the protection against external factors attribute of the Mitigating Systems cornerstone; and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding was evaluated using Phase 1 of Inspection Manual Chapter (IMC) 0609 Appendix F, Fire Protection Significance Determination Process. The inspectors determined that this issue was of very low safety significance because the degradation of the fire barrier was moderate based on the fire door displaying significant degradation affecting its performance or reliability.


However, it was still expected to provide some defense-in-depth benefit. Specifically, the fire door was expected to provide a minimum of 20 minutes fire endurance protection, and the in-situ fire ignition sources and flammable materials were positioned such that the degraded fire door would not be subject to direct flame impingement.
However, it was still expected to provide some defense-in-depth benefit. Specifically, the fire door was expected to provide a minimum of 20 minutes fire endurance protection, and the in-situ fire ignition sources and flammable materials were positioned such that the degraded fire door would not be subject to direct flame impingement.


The inspectors determined that the finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy personnel who routinely traverse through or past the fire door had not identified the degraded condition. (P.1(a))
The inspectors determined that the finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy personnel who routinely traverse through or past the fire door had not identified the degraded condition. (P.1(a))  
(Section 1R05)
(Section 1R05)
: '''Green.'''
: '''Green.'''
The inspectors identified a non-cited violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because Entergy did not ensure ivthat procedures associated with operation of the safety injection (SI) system during venting were appropriate to the circumstances. Specifically, procedure 2-PT-M108,  
The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,
"RHR/SI [residual heat removal/safety injection] System Venting," did not have appropriate controls to ensure the safety injection piping and pumps remained operable during accident conditions. Entergy entered the issue into their corrective action program and revised the venting procedure to ensure operator actions are appropriately evaluated and credited to maintain operability of the system.
Criterion V, Instructions, Procedures, and Drawings, because Entergy did not ensure iv that procedures associated with operation of the safety injection (SI) system during venting were appropriate to the circumstances. Specifically, procedure 2-PT-M108,
RHR/SI [residual heat removal/safety injection] System Venting, did not have appropriate controls to ensure the safety injection piping and pumps remained operable during accident conditions. Entergy entered the issue into their corrective action program and revised the venting procedure to ensure operator actions are appropriately evaluated and credited to maintain operability of the system.


The inspectors determined that this finding was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone; and it impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding was evaluated using Phase 1 of IMC 0609,
The inspectors determined that this finding was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone; and it impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding was evaluated using Phase 1 of IMC 0609,
Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations.The inspectors determined this finding resulted in a loss of function of a single train of SI for approximately five minutes. Because the total inoperability time was less than the allowed outage time of 72 hours, and the finding is not potentially risk significant due to a seismic, flooding, or severe weather initiating event, this finding screens as very low safety significance (Green).
Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations. The inspectors determined this finding resulted in a loss of function of a single train of SI for approximately five minutes. Because the total inoperability time was less than the allowed outage time of 72 hours, and the finding is not potentially risk significant due to a seismic, flooding, or severe weather initiating event, this finding screens as very low safety significance (Green).


The inspectors determined that this finding had a cross-cutting aspect in the area of human performance because Entergy did not ensure that complete, accurate and up-to-date procedures were available. (H.2(c)) (Section 1R22)  
The inspectors determined that this finding had a cross-cutting aspect in the area of human performance because Entergy did not ensure that complete, accurate and up-to-date procedures were available. (H.2(c)) (Section 1R22)  


===Cornerstone: Barrier Integrity===
===Cornerstone: Barrier Integrity===
: '''Green.'''
: '''Green.'''
The inspectors identified a non-cited violation of 10 CFR 50 Appendix B, Criterion XVI, "Corrective Actions," in that, Entergy did not implement timely corrective actions for a degraded condition associated with the 25 Containment Fan Cooler Unit (FCU) flow indicator. Specifically, the failure to take timely corrective actions for the degraded service water flow indicator for the 25 FCU, initially identified in October 2006, resulted in the inability to ensure that sufficient service water flow was available for the component to perform its intended function. Subsequently, it was identified that a reduced service water flow condition did exist. Entergy entered the issue into their corrective action program and implemented corrective actions to restore adequate indication of service water flow to the 25 FCU. Entergy is evaluating maintenance practices to determine the appropriateness of a periodic blow-down of the transmitter impulse lines to prevent sediment buildup.
The inspectors identified a non-cited violation of 10 CFR 50 Appendix B,
Criterion XVI, Corrective Actions, in that, Entergy did not implement timely corrective actions for a degraded condition associated with the 25 Containment Fan Cooler Unit (FCU) flow indicator. Specifically, the failure to take timely corrective actions for the degraded service water flow indicator for the 25 FCU, initially identified in October 2006, resulted in the inability to ensure that sufficient service water flow was available for the component to perform its intended function. Subsequently, it was identified that a reduced service water flow condition did exist. Entergy entered the issue into their corrective action program and implemented corrective actions to restore adequate indication of service water flow to the 25 FCU. Entergy is evaluating maintenance practices to determine the appropriateness of a periodic blow-down of the transmitter impulse lines to prevent sediment buildup.
 
The inspectors determined that this finding was more than minor because it was associated with the structure, system, and component and barrier performance attribute of the Barrier Integrity cornerstone; and it impacted the cornerstone objective of providing reasonable assurance that the physical design barrier (containment) protects the public from radionuclide releases caused by accidents or events. This finding was evaluated using IMC 0609, Appendix H, Containment Integrity Significance Determination Process. This was determined to be a Type B finding because it potentially impacted containment integrity but did not result in the increased likelihood of an initiating event. This finding was determined to be of very low safety significance v because, while it could impact late containment failure, it did not impact a function that was important to large early release frequency.
 
The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy did not thoroughly evaluate the condition when initially identified. (P.1(c)) (Section 1R13)


The inspectors determined that this finding was more than minor because it was associated with the structure, system, and component and barrier performance attribute of the Barrier Integrity cornerstone; and it impacted the cornerstone objective of providing reasonable assurance that the physical design barrier (containment) protects the public from radionuclide releases caused by accidents or events. This finding was evaluated using IMC 0609, Appendix H, "Containment Integrity Significance Determination Process."  This was determined to be a Type B finding because it potentially impacted containment integrity but did not result in the increased likelihood of an initiating event. This finding was determined to be of very low safety significance vbecause, while it could impact late containment failure, it did not impact a function that was important to large early release frequency.
B.


The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy did not thoroughly evaluate the condition when initially identified.  (P.1(c))  (Section 1R13)
Licensee-Identified Violation


B. Licensee-Identified Violation None.
None.


=REPORT DETAILS=
=REPORT DETAILS=


===Summary of Plant Status===
===Summary of Plant Status===
Indian Point Nuclear Generating Unit 2 began the inspection period operating at full power and remained at or near full power throughout the inspection period.
Indian Point Nuclear Generating Unit 2 began the inspection period operating at full power and remained at or near full power throughout the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
{{a|1R01}}


{{a|1R01}}
==1R01 Adverse Weather Protection==
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01|count=1}}
{{IP sample|IP=IP 71111.01|count=1}}
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No findings of significance were identified.
No findings of significance were identified.


{{a|1R04}}
{{a|1R04}}
 
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04Q|count=3}}
{{IP sample|IP=IP 71111.04Q|count=3}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial system walkdowns to verify the operability of redundant or diverse trains and components during periods of system train unavailability or following periods of maintenance. The inspectors referenced the system procedures, the Updated Final Safety Analysis Report (UFSAR), and system drawings to verify that the alignment of the available train supported its required safety functions. The inspectors also reviewed applicable condition reports and work orders to ensure that Entergy had identified and properly addressed equipment discrepancies that could potentially impair the capability of the available train, as required by Title 10 of the Code of Federal Regulations (CFR) Part 50, Appendix B, Criterion XVI, "Corrective Action."
The inspectors performed partial system walkdowns to verify the operability of redundant or diverse trains and components during periods of system train unavailability or following periods of maintenance. The inspectors referenced the system procedures, the Updated Final Safety Analysis Report (UFSAR), and system drawings to verify that the alignment of the available train supported its required safety functions. The inspectors also reviewed applicable condition reports and work orders to ensure that Entergy had identified and properly addressed equipment discrepancies that could potentially impair the capability of the available train, as required by Title 10 of the Code of Federal Regulations (CFR) Part 50, Appendix B, Criterion XVI, Corrective Action.


The documents reviewed during these inspections are listed in the Attachment.
The documents reviewed during these inspections are listed in the Attachment.


The inspectors performed partial walkdowns on the following systems which represented three inspection samples:
The inspectors performed partial walkdowns on the following systems which represented three inspection samples:
* 21, 22 and 23 emergency diesel generators (EDG's) during severe weather warning and elevated risk;
* 21, 22 and 23 emergency diesel generators (EDGs) during severe weather warning and elevated risk;
* Emergency diesel generator alignment during 480 Volt undervoltage testing; and
* Emergency diesel generator alignment during 480 Volt undervoltage testing; and
* Fire protection system following 11 fire main booster pump testing.
* Fire protection system following 11 fire main booster pump testing.
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No findings of significance were identified.
No findings of significance were identified.


{{a|1R05}}
{{a|1R05}}
 
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05Q|count=10}}
{{IP sample|IP=IP 71111.05Q|count=10}}


===.1 Quarterly Inspection===
===.1 Quarterly Inspection===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted a tour of several fire areas to assess the material condition and operational status of fire protection features. The inspectors verified, consistent with applicable administrative procedures, that: combustibles and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with Entergy's fire protection program. The inspectors evaluated the fire protection program against the requirements of Licensee Condition 2.K. The documents reviewed are listed in the Attachment. This inspection represented 10 inspection samples for fire protection tours and were conducted in the following areas:
The inspectors conducted a tour of several fire areas to assess the material condition and operational status of fire protection features. The inspectors verified, consistent with applicable administrative procedures, that: combustibles and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with Entergys fire protection program. The inspectors evaluated the fire protection program against the requirements of Licensee Condition 2.K. The documents reviewed are listed in the Attachment. This inspection represented 10 inspection samples for fire protection tours and were conducted in the following areas:
* Fire Zone 23;
* Fire Zone 23;
* Fire Zone 10;
* Fire Zone 10;
Line 162: Line 169:


====b. Findings====
====b. Findings====
=====Introduction:=====
=====Introduction:=====
The inspectors identified a Green non-cited violation (NCV) of License Condition 2.K., fire protection program, because Entergy failed to identify a degraded three-hour rated fire door on the east entrance of the 12 fire main booster pump room.
The inspectors identified a Green non-cited violation (NCV) of License Condition 2.K., fire protection program, because Entergy failed to identify a degraded three-hour rated fire door on the east entrance of the 12 fire main booster pump room.


=====Description:=====
=====Description:=====
On September 6, 2007, the inspectors performed a fire protection walkdown of the 11 and 12 fire main booster pump areas. The inspectors noted that the three-hour rated, swing-type fire door on the east side of the 12 fire main booster pump cell would not close properly and left a gap along the perimeter of the door. The inspectors reviewed Entergy's Fire Hazards Analysis Report and determined that the door is required to meet licensing commitments, and is designed to preclude the passage of flame and hot gases from the adjacent area. Degradation of this door could allow the propagation of a fire to impact the 12 fire main booster pump.
On September 6, 2007, the inspectors performed a fire protection walkdown of the 11 and 12 fire main booster pump areas. The inspectors noted that the three-hour rated, swing-type fire door on the east side of the 12 fire main booster pump cell would not close properly and left a gap along the perimeter of the door. The inspectors reviewed Entergys Fire Hazards Analysis Report and determined that the door is required to meet licensing commitments, and is designed to preclude the passage of flame and hot gases from the adjacent area. Degradation of this door could allow the propagation of a fire to impact the 12 fire main booster pump.


The inspectors informed shift operations personnel of the issue, and they determined the door was improperly aligned with the frame. Entergy evaluated the condition, took appropriate compensatory measures, realigned the door, ensured that it would fully close, and entered the condition into their corrective action program (CR-IP2-2007-03561). Additionally, the fire protection engineer was notified, and he determined that the door frame required replacement (CR-IP2-2007-03651).
The inspectors informed shift operations personnel of the issue, and they determined the door was improperly aligned with the frame. Entergy evaluated the condition, took appropriate compensatory measures, realigned the door, ensured that it would fully close, and entered the condition into their corrective action program (CR-IP2-2007-03561). Additionally, the fire protection engineer was notified, and he determined that the door frame required replacement (CR-IP2-2007-03651).


The inspectors determined that this condition was a performance deficiency because the door was in a degraded condition that resulted in the fire barrier being non-functional. The inspectors determined it was reasonable that this condition should have been identified by Entergy because personnel routinely pass through the fire door, and the inability of the door to fully close was readily apparent. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRC's regulatory function, and the finding was not the result of any willful violation of NRC requirements.
The inspectors determined that this condition was a performance deficiency because the door was in a degraded condition that resulted in the fire barrier being non-functional. The inspectors determined it was reasonable that this condition should have been identified by Entergy because personnel routinely pass through the fire door, and the inability of the door to fully close was readily apparent. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRCs regulatory function, and the finding was not the result of any willful violation of NRC requirements.


=====Analysis:=====
=====Analysis:=====
The inspectors determined that this finding was more than minor because it was associated with the protection against external factors attribute of the Mitigating Systems cornerstone; and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors performed a Phase 1 screening of the deficiency in accordance with Inspection Manual Chapter (IMC) 0609 and evaluated the safety-significance using IMC 0609 Appendix F, "Fire Protection Significance Determination Process.The issue was determined to be of very low safety significance because the degradation of the fire barrier was "moderate" based on the fire door displaying significant degradation affecting its performance or reliability. However, it was still expected to provide some defense-in-depth benefit. Specifically, the fire door was expected to provide a minimum of 20 minutes fire endurance protection, and the in-situ fire ignition sources and flammable materials were positioned such that the degraded fire door would not be subject to direct flame impingement.
The inspectors determined that this finding was more than minor because it was associated with the protection against external factors attribute of the Mitigating Systems cornerstone; and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors performed a Phase 1 screening of the deficiency in accordance with Inspection Manual Chapter (IMC) 0609 and evaluated the safety-significance using IMC 0609 Appendix F, Fire Protection Significance Determination Process. The issue was determined to be of very low safety significance because the degradation of the fire barrier was moderate based on the fire door displaying significant degradation affecting its performance or reliability. However, it was still expected to provide some defense-in-depth benefit. Specifically, the fire door was expected to provide a minimum of 20 minutes fire endurance protection, and the in-situ fire ignition sources and flammable materials were positioned such that the degraded fire door would not be subject to direct flame impingement.


The inspectors determined that the finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy personnel who routinely traverse through or past the fire door had not identified the degraded condition. (P.1(a))  
The inspectors determined that the finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy personnel who routinely traverse through or past the fire door had not identified the degraded condition. (P.1(a))  


=====Enforcement:=====
=====Enforcement:=====
License Condition 2.K., fire protection program, requires that Entergy implement and maintain in effect all provisions of the NRC-approved fire protection program, as approved in part by the NRC Safety Evaluation Report (SER) dated January 31, 1979. The January 31, 1979, SER requires administrative controls comparable to those described in NRC Branch Technical Position 9.5-1, "Guidelines for Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976.Branch Technical Position (BTP) 9.5-1 requires that measures be established to assure that conditions adverse to fire protection, such as deficiencies, deviations, defective components, and non-conformities are promptly identified, reported, and corrected.
License Condition 2.K., fire protection program, requires that Entergy implement and maintain in effect all provisions of the NRC-approved fire protection program, as approved in part by the NRC Safety Evaluation Report (SER) dated January 31, 1979. The January 31, 1979, SER requires administrative controls comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch Technical Position (BTP) 9.5-1 requires that measures be established to assure that conditions adverse to fire protection, such as deficiencies, deviations, defective components, and non-conformities are promptly identified, reported, and corrected.
 
Contrary to the above, Entergy failed to promptly identify the degraded condition of the 12 fire main booster pump area fire door. Once identified by the inspectors, Entergy initiated CRs IP2-2007-03561 and IP2-2007-03651 documenting the deficiency in their corrective action program (CAP). Because the violation was of very low safety significance and entered into their CAP, this violation is being treated as an NCV per Section VI.A of the NRC Enforcement Policy: NCV 05000247/2007004-01, Degraded 12 Fire Main Booster Pump Cell Fire Door.


Contrary to the above, Entergy failed to promptly identify the degraded condition of the 12 fire main booster pump area fire door. Once identified by the inspectors, Entergy initiated CRs IP2-2007-03561 and IP2-2007-03651 documenting the deficiency in their corrective action program (CAP). Because the violation was of very low safety significance and entered into their CAP, this violation is being treated as an NCV per Section VI.A of the NRC Enforcement Policy:  NCV 05000247/2007004-01, Degraded 12 Fire Main Booster Pump Cell Fire Door.
{{a|1R06}}
{{a|1R06}}
==1R06 Flood Protection Measures==
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06|count=1}}
{{IP sample|IP=IP 71111.06|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed Indian Point Nuclear Generating Unit 2's Individual Plant Examination and the UFSAR concerning internal flooding events. The inspection included a walkdown of accessible areas of the plant, including the service water pipe chase area of the primary auxiliary building. Inspectors evaluated these areas for potential susceptibilities to internal flooding and verified the assumptions included in the site's internal flooding analysis. The inspectors also reviewed relevant abnormal operating and emergency plan procedures. The documents reviewed are listed in the  
The inspectors reviewed Indian Point Nuclear Generating Unit 2s Individual Plant Examination and the UFSAR concerning internal flooding events. The inspection included a walkdown of accessible areas of the plant, including the service water pipe chase area of the primary auxiliary building. Inspectors evaluated these areas for potential susceptibilities to internal flooding and verified the assumptions included in the sites internal flooding analysis. The inspectors also reviewed relevant abnormal operating and emergency plan procedures. The documents reviewed are listed in the  
. This inspection represented one sample for internal flood protection measures.
. This inspection represented one sample for internal flood protection measures.


====b. Findings====
====b. Findings====
No findings of significance were identified.  
No findings of significance were identified.
{{a|1R11}}
 
{{a|1R11}}
 
==1R11 Licensed Operator Requalification Program==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11Q|count=1}}
{{IP sample|IP=IP 71111.11Q|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
On August 20, 2007, the inspectors observed licensed operator simulator training to verify that operator performance was adequate and that evaluators were identifying and documenting crew performance problems. The inspectors evaluated the performance of risk-significant operator actions, including the use of emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operation and manipulation, and the oversight and direction provided by the shift manager. The inspectors also reviewed simulator fidelity with respect to the actual plant. Licensed operator training was evaluated against the requirements of 10 CFR Part 55, "Operators' Licenses.The documents reviewed during this inspection are listed in the Attachment. This observation of operator simulator training represented one inspection sample.
On August 20, 2007, the inspectors observed licensed operator simulator training to verify that operator performance was adequate and that evaluators were identifying and documenting crew performance problems. The inspectors evaluated the performance of risk-significant operator actions, including the use of emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operation and manipulation, and the oversight and direction provided by the shift manager. The inspectors also reviewed simulator fidelity with respect to the actual plant. Licensed operator training was evaluated against the requirements of 10 CFR Part 55, Operators Licenses. The documents reviewed during this inspection are listed in the Attachment. This observation of operator simulator training represented one inspection sample.


====b. Findings====
====b. Findings====
No findings of significance were identified.  
No findings of significance were identified.
{{a|1R12}}
 
{{a|1R12}}
 
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12Q|count=3}}
{{IP sample|IP=IP 71111.12Q|count=3}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed performance-based problems that involved the selected structures, systems, or components (SSC's) to assess the effectiveness of the maintenance program. Reviews focused on:
The inspectors reviewed performance-based problems that involved the selected structures, systems, or components (SSCs) to assess the effectiveness of the maintenance program. Reviews focused on:
* Proper Maintenance Rule scoping in accordance with 10 CFR 50.65;
* Proper Maintenance Rule scoping in accordance with 10 CFR 50.65;
* Characterization of reliability issues;
* Characterization of reliability issues;
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* Service water piping and system leaks;
* Service water piping and system leaks;
* Direct Current (DC) power; and
* Direct Current (DC) power; and
* Appendix 'R' lighting.
* Appendix R lighting.


====b. Findings====
====b. Findings====
No findings of significance were identified.  
No findings of significance were identified.
{{a|1R13}}
 
{{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=5}}
{{IP sample|IP=IP 71111.13|count=5}}
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The inspectors reviewed maintenance activities to verify that the appropriate risk assessments were performed prior to removing equipment for work. The inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The documents reviewed during this inspection are listed in the Attachment.
The inspectors reviewed maintenance activities to verify that the appropriate risk assessments were performed prior to removing equipment for work. The inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The documents reviewed during this inspection are listed in the Attachment.


6The following activities represented five inspection samples:
The following activities represented five inspection samples:
* 21 safety injection pump maintenance during 22 residual heat removal pump testing;
* 21 safety injection pump maintenance during 22 residual heat removal pump testing;
* Decreased indicated service water flow to 25 containment fan cooler unit;
* Decreased indicated service water flow to 25 containment fan cooler unit;
* 22 auxiliary feedwater pump planned maintenance;
* 22 auxiliary feedwater pump planned maintenance;
* 345 KiloVolt (KV) feeder W93 removed from service; and
* 345 KiloVolt (KV) feeder W93 removed from service; and
* Rod control circuit QC-412B replacement.
* Rod control circuit QC-412B replacement.


====b. Findings====
====b. Findings====
=====Introduction:=====
=====Introduction:=====
The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," in that, Entergy did not implement timely corrective actions for a degraded condition associated with the 25 containment fan cooler unit (FCU) service water flow indication.
The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, in that, Entergy did not implement timely corrective actions for a degraded condition associated with the 25 containment fan cooler unit (FCU) service water flow indication.


Discussion: On September 16, 2007, Entergy conducted a quarterly surveillance to verify adequate cooling water flow through the containment FCUs. Entergy identified that the 25 FCU did not meet the minimum required flow, and declared the FCU inoperable. Entergy initiated corrective actions to restore flow to greater than the minimum required by Technical Specifications, and the 25 FCU was restored to an operable status on September 20, 2007.
Discussion: On September 16, 2007, Entergy conducted a quarterly surveillance to verify adequate cooling water flow through the containment FCUs. Entergy identified that the 25 FCU did not meet the minimum required flow, and declared the FCU inoperable. Entergy initiated corrective actions to restore flow to greater than the minimum required by Technical Specifications, and the 25 FCU was restored to an operable status on September 20, 2007.


The inspectors evaluated Entergy's actions to restore adequate flow to the 25 FCU and reviewed the associated risk management actions during the emergent work. In addition, the inspectors reviewed the past work history associated with service water flow to the FCU. The inspectors identified that a condition report, CR-IP2-2006-05951, had been written on October 8, 2006, due to anomalous service water flow indications on 25 FCU during a valve stroke surveillance test. This issue was evaluated in the corrective action process, and it was determined that the most likely cause for the oscillating indication was excessive silting of the instrument lines to the flow transmitter.
The inspectors evaluated Entergys actions to restore adequate flow to the 25 FCU and reviewed the associated risk management actions during the emergent work. In addition, the inspectors reviewed the past work history associated with service water flow to the FCU. The inspectors identified that a condition report, CR-IP2-2006-05951, had been written on October 8, 2006, due to anomalous service water flow indications on 25 FCU during a valve stroke surveillance test. This issue was evaluated in the corrective action process, and it was determined that the most likely cause for the oscillating indication was excessive silting of the instrument lines to the flow transmitter.


A work order was written to blowdown the instrument lines associated with the transmitter, and the condition report was closed to the work order. The work order was coded as elective maintenance because Entergy determined that the deficiency was only associated with the flow indication, and did not represent an actual reduction in flow. This work order was not implemented. Entergy failed to consider that the valve alignment for the test in which the anomaly was identified was the same alignment as required by the quarterly surveillance to verify adequate service water flow to the containment fan cooler units. Condition report, CR-IP2-2007-03424, was written on August 28, 2007, that identified the same anomalous flow condition and a corrective action to blowdown the impulse lines was completed on August 30, 2007.
A work order was written to blowdown the instrument lines associated with the transmitter, and the condition report was closed to the work order. The work order was coded as elective maintenance because Entergy determined that the deficiency was only associated with the flow indication, and did not represent an actual reduction in flow. This work order was not implemented. Entergy failed to consider that the valve alignment for the test in which the anomaly was identified was the same alignment as required by the quarterly surveillance to verify adequate service water flow to the containment fan cooler units. Condition report, CR-IP2-2007-03424, was written on August 28, 2007, that identified the same anomalous flow condition and a corrective action to blowdown the impulse lines was completed on August 30, 2007.
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The inspectors reviewed the data obtained during the quarterly surveillance test for periods before, and after the anomalous flow condition was identified in October 2006.
The inspectors reviewed the data obtained during the quarterly surveillance test for periods before, and after the anomalous flow condition was identified in October 2006.


Prior to the anomaly being identified, the flow for 25 FCU was routinely found to be in the range of 1760-1800 gallons per minute (gpm). After October 2006, the flow was recorded as being greater than 2000 gpm, with the exception of one instance where the 7flow was 1780 gpm. 2000 gpm is the maximum value in the indicating range of the meter. The inspectors determined that, based on the identified anomaly in the flow indication and the prompt change in indicated flow during the quarterly surveillance, the meter did not provide a reliable indication of actual system flow. Entergy determined that the actual reduction in service water flow through the 25 FCU identified on September 16, 2007, was the result of flow blockage in the system and most likely occurred during heavy rains, and a subsequent increase in river water silt and debris, during April 2007. The inspectors determined that the unreliable service water flow indication prevented earlier indication of the flow reduction through the quarterly surveillance test. Entergy implemented corrective actions to restore adequate service water flow indication to 25 FCU and is evaluating maintenance practices to determine the appropriateness of a periodic blowdown of the transmitter impulse lines to prevent sediment buildup.
Prior to the anomaly being identified, the flow for 25 FCU was routinely found to be in the range of 1760-1800 gallons per minute (gpm). After October 2006, the flow was recorded as being greater than 2000 gpm, with the exception of one instance where the flow was 1780 gpm. 2000 gpm is the maximum value in the indicating range of the meter. The inspectors determined that, based on the identified anomaly in the flow indication and the prompt change in indicated flow during the quarterly surveillance, the meter did not provide a reliable indication of actual system flow. Entergy determined that the actual reduction in service water flow through the 25 FCU identified on September 16, 2007, was the result of flow blockage in the system and most likely occurred during heavy rains, and a subsequent increase in river water silt and debris, during April 2007. The inspectors determined that the unreliable service water flow indication prevented earlier indication of the flow reduction through the quarterly surveillance test. Entergy implemented corrective actions to restore adequate service water flow indication to 25 FCU and is evaluating maintenance practices to determine the appropriateness of a periodic blowdown of the transmitter impulse lines to prevent sediment buildup.


The inspectors determined that the failure to take timely corrective action for a degraded condition was a performance deficiency and did not meet the requirements of 10 CFR 50 Appendix B, Criterion XVI, "Corrective Actions.The cause of this performance deficiency was within Entergy's ability to foresee and prevent, because Entergy did not fully evaluate anomalous flow indications on the 25 FCU in October 2006 and subsequent changes in flow rate during quarterly surveillance testing. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRC's regulatory function, and the finding was not the result of any willful violation of NRC requirements or Entergy's procedures.
The inspectors determined that the failure to take timely corrective action for a degraded condition was a performance deficiency and did not meet the requirements of 10 CFR 50 Appendix B, Criterion XVI, Corrective Actions. The cause of this performance deficiency was within Entergys ability to foresee and prevent, because Entergy did not fully evaluate anomalous flow indications on the 25 FCU in October 2006 and subsequent changes in flow rate during quarterly surveillance testing. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRCs regulatory function, and the finding was not the result of any willful violation of NRC requirements or Entergys procedures.


=====Analysis:=====
=====Analysis:=====
The inspectors determined that this finding was more than minor because it was associated with the SSC and barrier performance attribute of the Barrier Integrity cornerstone; and it impacted the cornerstone objective of providing reasonable assurance that the physical design barrier (containment) protects the public from radionuclide releases caused by accidents or events. Specifically, the failure to take timely corrective actions for the degraded service water flow indicator for the 25 FCU, initially identified in October 2006, resulted in the inability to ensure that sufficient service water flow was available for the FCU to perform its intended safety function.
The inspectors determined that this finding was more than minor because it was associated with the SSC and barrier performance attribute of the Barrier Integrity cornerstone; and it impacted the cornerstone objective of providing reasonable assurance that the physical design barrier (containment) protects the public from radionuclide releases caused by accidents or events. Specifically, the failure to take timely corrective actions for the degraded service water flow indicator for the 25 FCU, initially identified in October 2006, resulted in the inability to ensure that sufficient service water flow was available for the FCU to perform its intended safety function.


Subsequently, it was identified that a reduced service water flow condition did exist. The inspectors evaluated this finding using IMC 0609, Appendix H, "Containment Integrity Significance Determination Process.This was determined to be a Type B finding because it potentially impacted containment integrity but did not result in the increased likelihood of an initiating event. This finding was determined to be of very low safety significance because, while it could impact late containment failure, it did not impact a function that was important to large early release frequency.
Subsequently, it was identified that a reduced service water flow condition did exist. The inspectors evaluated this finding using IMC 0609, Appendix H, Containment Integrity Significance Determination Process. This was determined to be a Type B finding because it potentially impacted containment integrity but did not result in the increased likelihood of an initiating event. This finding was determined to be of very low safety significance because, while it could impact late containment failure, it did not impact a function that was important to large early release frequency.


The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy did not thoroughly evaluate the condition when initially identified. Specifically, the evaluation did not address the impact of the degraded condition on the flow indication obtained during the quarterly surveillance, which ensures adequate service water flow. Therefore, the work order to blow-down the instrument lines was not appropriately prioritized to ensure the corrective action was performed in a timely manner. (P.1(c))
The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy did not thoroughly evaluate the condition when initially identified. Specifically, the evaluation did not address the impact of the degraded condition on the flow indication obtained during the quarterly surveillance, which ensures adequate service water flow. Therefore, the work order to blow-down the instrument lines was not appropriately prioritized to ensure the corrective action was performed in a timely manner. (P.1(c))  


=====Enforcement:=====
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected. Contrary to the above, Entergy failed to correct a condition adverse to quality in a prompt manner, commensurate with its safety significance. Specifically, the corrective actions associated with the degraded service water flow indication, initially identified in October 2006, were not performed in a timely manner and resulted in the inability to promptly identify an actual degradation of service water flow to 25 FCU. Because of the very low safety significance of this finding and because the finding was entered into Entergy's corrective action program as CR-IP2-2007-03706, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected. Contrary to the above, Entergy failed to correct a condition adverse to quality in a prompt manner, commensurate with its safety significance. Specifically, the corrective actions associated with the degraded service water flow indication, initially identified in October 2006, were not performed in a timely manner and resulted in the inability to promptly identify an actual degradation of service water flow to 25 FCU. Because of the very low safety significance of this finding and because the finding was entered into Entergys corrective action program as CR-IP2-2007-03706, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000247/2007004-02, Untimely Corrective Actions to Repair a Degraded Service Water Flow Instrument.
NCV 05000247/2007004-02, Untimely Corrective Actions to Repair a Degraded Service Water Flow Instrument.


{{a|1R15}}
{{a|1R15}}
==1R15 Operability Evaluations==
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15|count=5}}
{{IP sample|IP=IP 71111.15|count=5}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications. The inspectors' reviews included verification that the operability determinations were performed in accordance with procedure ENN-OP-104, "Operability Determinations." The inspectors assessed the technical adequacy of the evaluations to ensure consistency with the Technical Specifications, UFSAR, and associated design basis documents. The documents reviewed during this inspection are listed in the Attachment. The following operability evaluations were reviewed and represented five inspection samples:
The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications. The inspectors' reviews included verification that the operability determinations were performed in accordance with procedure ENN-OP-104, "Operability Determinations." The inspectors assessed the technical adequacy of the evaluations to ensure consistency with the Technical Specifications, UFSAR, and associated design basis documents. The documents reviewed during this inspection are listed in the Attachment. The following operability evaluations were reviewed and represented five inspection samples:
* CR IP2-07-02514, Service water pipe chase leak in the vicinity of SWN-840;
* CR IP2-07-02514, Service water pipe chase leak in the vicinity of SWN-840;
* CR IP2-07-03226, Service water leak downstream of SWN 71-5B;
* CR IP2-07-03226, Service water leak downstream of SWN 71-5B;
* CR IP2-07-03161, 23 Station battery charger found below TS surveillance criteria;
* CR IP2-07-03161, 23 Station battery charger found below TS surveillance criteria;
* CR IP2-2007-03275, Potential to hydraulic lock containment sump recirculation valves (IP2 & 3); and
* CR IP2-2007-03275, Potential to hydraulic lock containment sump recirculation valves (IP2 & 3); and
* CR IP2-2007-03820, Service water leak upstream SWN-46.
* CR IP2-2007-03820, Service water leak upstream SWN-46.


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No findings of significance were identified.
No findings of significance were identified.


91R19 Post-Maintenance Testing (71111.19 - 6 samples)
{{a|1R19}}
 
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and engineering personnel. The inspectors verified: test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Upon completion, the inspectors verified that equipment was returned to the proper alignment necessary to perform its safety function.
The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and engineering personnel. The inspectors verified: test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Upon completion, the inspectors verified that equipment was returned to the proper alignment necessary to perform its safety function.


Post-maintenance testing was evaluated against the requirements of 10 CFR Part 50, Appendix B, Criterion XI, "Test Control.The documents reviewed during this inspection are listed in the Attachment. The following post-maintenance activities were reviewed and represented six inspection samples:
Post-maintenance testing was evaluated against the requirements of 10 CFR Part 50, Appendix B, Criterion XI, Test Control. The documents reviewed during this inspection are listed in the Attachment. The following post-maintenance activities were reviewed and represented six inspection samples:
* WO IP2-06-26506, 23 coolant charging pump following mechanical seal replacement;
* WO IP2-06-26506, 23 coolant charging pump following mechanical seal replacement;
* WO 51322853, recirculation sump LT 3301 replacement;
* WO 51322853, recirculation sump LT 3301 replacement;
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====b. Findings====
====b. Findings====
No findings of significance were identified.  
No findings of significance were identified.
{{a|1R22}}
 
{{a|1R22}}
 
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=5}}
{{IP sample|IP=IP 71111.22|count=5}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors witnessed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems and components to assess whether they satisfied Technical Specifications, UFSAR, Technical Requirements Manual, and Entergy procedure requirements. The inspectors verified that: test acceptance criteria were clear, demonstrated operational readiness, and were consistent with design basis documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Following the test, the inspectors verified that the equipment was capable of performing the required safety functions. The inspectors evaluated the surveillance tests against the requirements in Technical Specifications. The documents 10reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented five inspection samples:
The inspectors witnessed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems and components to assess whether they satisfied Technical Specifications, UFSAR, Technical Requirements Manual, and Entergy procedure requirements. The inspectors verified that: test acceptance criteria were clear, demonstrated operational readiness, and were consistent with design basis documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Following the test, the inspectors verified that the equipment was capable of performing the required safety functions. The inspectors evaluated the surveillance tests against the requirements in Technical Specifications. The documents reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented five inspection samples:
* 2-PT-Q16, "Containment fan cooler unit cooling water test;"
* 2-PT-Q16, Containment fan cooler unit cooling water test;
* 2-PT-M7, "Analog rod position functional test;"
* 2-PT-M7, Analog rod position functional test;
* 2-PT-27A, "22 Auxiliary feed water pump;"
* 2-PT-27A, 22 Auxiliary feed water pump;
* 2-PT-M108, "Emergency core cooling system venting;" and
* 2-PT-M108, Emergency core cooling system venting; and
* 0-SOP-LEAKRATE-001, "Reactor coolant system leakrate surveillance, evaluation and identification."
* 0-SOP-LEAKRATE-001, Reactor coolant system leakrate surveillance, evaluation and identification.


====b. Findings====
====b. Findings====
=====Introduction:=====
=====Introduction:=====
The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because Entergy did not ensure that procedures associated with operation of the safety injection (SI) system during venting were appropriate to the circumstances.
The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, because Entergy did not ensure that procedures associated with operation of the safety injection (SI) system during venting were appropriate to the circumstances.


=====Description:=====
=====Description:=====
During observation of a monthly operations procedure to perform safety injection system venting in accordance with procedure 2-PT-M108, "RHR/SI [residual heat removal/safety injection] System Venting," the inspectors noted the licensee did not declare the pumps or various safety injection subsystems inoperable during the actual venting process. In the case of the SI pump, which is vented every month, the procedure assumes the pump is operable. The inspectors questioned whether the pump remained operable with the casing vent open because some flow would not be available for core injection, and on sump recirculation the emergency core cooling system (ECCS) leakage outside the containment could be high. Entergy determined that the pump would not fulfill its safety function if the valve was left in the full open position. The inspectors reviewed the procedures to determine if credit would be reasonable for the operator to perform this manual action to close the valve instead of the function of the SI system to respond automatically. There were no procedure requirements in place to ensure that a dedicated operator would be present, in constant communication, and with appropriate guidance to take actions as needed if an event was to occur during the venting evolution. The inspectors concluded the pump should not be considered operable, because crediting manual operator action in lieu of the pump running automatically requires consideration of the manual actions needed to restore operability and reviewing them pursuant to 10 CFR 50.59. In addition, other possible piping vent paths are used in the procedure. Although these vents would only be used if gas voids are found in certain locations, there is a potential the vent could be used as the procedure directs. The procedure guidance for these paths was also deficient; crediting the operator to perform an action to ensure the SI system retained its safety function. The licensee wrote CR-IP2-2007-03032 to address these concerns.
During observation of a monthly operations procedure to perform safety injection system venting in accordance with procedure 2-PT-M108, RHR/SI [residual heat removal/safety injection] System Venting, the inspectors noted the licensee did not declare the pumps or various safety injection subsystems inoperable during the actual venting process. In the case of the SI pump, which is vented every month, the procedure assumes the pump is operable. The inspectors questioned whether the pump remained operable with the casing vent open because some flow would not be available for core injection, and on sump recirculation the emergency core cooling system (ECCS) leakage outside the containment could be high. Entergy determined that the pump would not fulfill its safety function if the valve was left in the full open position. The inspectors reviewed the procedures to determine if credit would be reasonable for the operator to perform this manual action to close the valve instead of the function of the SI system to respond automatically. There were no procedure requirements in place to ensure that a dedicated operator would be present, in constant communication, and with appropriate guidance to take actions as needed if an event was to occur during the venting evolution. The inspectors concluded the pump should not be considered operable, because crediting manual operator action in lieu of the pump running automatically requires consideration of the manual actions needed to restore operability and reviewing them pursuant to 10 CFR 50.59. In addition, other possible piping vent paths are used in the procedure. Although these vents would only be used if gas voids are found in certain locations, there is a potential the vent could be used as the procedure directs. The procedure guidance for these paths was also deficient; crediting the operator to perform an action to ensure the SI system retained its safety function. The licensee wrote CR-IP2-2007-03032 to address these concerns.


The licensee revised procedures, providing detailed guidance crediting operator action, or in the case for some piping vents, changed the procedure to ensure the valve was not opened such that excess SI flow would be lost during venting.
The licensee revised procedures, providing detailed guidance crediting operator action, or in the case for some piping vents, changed the procedure to ensure the valve was not opened such that excess SI flow would be lost during venting.


The inspectors concluded that the procedure lacked adequate guidance to ensure the SI system remained operable by controlling valve positions or having detailed instructions 11to credit an operator to perform these actions. Entergy implemented corrective actions and revised the venting procedure to ensure operator actions were appropriately evaluated and credited to maintain operability of the system.
The inspectors concluded that the procedure lacked adequate guidance to ensure the SI system remained operable by controlling valve positions or having detailed instructions to credit an operator to perform these actions. Entergy implemented corrective actions and revised the venting procedure to ensure operator actions were appropriately evaluated and credited to maintain operability of the system.


The inspectors determined that the failure to ensure that procedures associated with the venting of the SI lines were appropriate to the circumstances and included appropriate controls of plant equipment or dedicated operator was a performance deficiency and did not meet the requirements of 10 CFR 50 Appendix B, Criterion V, "Instructions, Procedures, and Drawing.The cause of this performance deficiency was within Entergy's ability to foresee and prevent, based on readily available NRC and industry guidance on maintaining the operability of systems during certain evolutions, such as venting. Traditional enforcement does not apply because there were no actual safety consequences or potential for impacting the NRC's regulatory function, and the finding was not the result of any willful violation of NRC requirements or Entergy's procedures.
The inspectors determined that the failure to ensure that procedures associated with the venting of the SI lines were appropriate to the circumstances and included appropriate controls of plant equipment or dedicated operator was a performance deficiency and did not meet the requirements of 10 CFR 50 Appendix B, Criterion V, Instructions, Procedures, and Drawing. The cause of this performance deficiency was within Entergys ability to foresee and prevent, based on readily available NRC and industry guidance on maintaining the operability of systems during certain evolutions, such as venting. Traditional enforcement does not apply because there were no actual safety consequences or potential for impacting the NRCs regulatory function, and the finding was not the result of any willful violation of NRC requirements or Entergys procedures.


=====Analysis:=====
=====Analysis:=====
The inspectors determined that this finding was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone; and it impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, procedure 2-PT-M108, "RHR/SI System Venting," did not have appropriate controls to ensure the SI piping and pumps remained operable during accident conditions. This finding was evaluated using Phase 1 of IMC 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations.The inspectors determined this finding resulted in a loss of function of a single train of SI for approximately five minutes. Because the total inoperability time was less than the allowed outage time of 72 hours, and the finding is not potentially risk significant due to a seismic, flooding, or severe weather initiating event, this finding screens as very low safety significance (Green).
The inspectors determined that this finding was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone; and it impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, procedure 2-PT-M108, RHR/SI System Venting, did not have appropriate controls to ensure the SI piping and pumps remained operable during accident conditions. This finding was evaluated using Phase 1 of IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations. The inspectors determined this finding resulted in a loss of function of a single train of SI for approximately five minutes. Because the total inoperability time was less than the allowed outage time of 72 hours, and the finding is not potentially risk significant due to a seismic, flooding, or severe weather initiating event, this finding screens as very low safety significance (Green).


The inspectors determined that this finding had a cross-cutting aspect in the area of human performance because Entergy did not ensure that complete, accurate and up-to-date procedures were available. Specifically, Entergy did not ensure that the venting procedure for the SI system had adequate guidance to ensure the SI system remained operable by controlling valve positions, or having detailed instructions to credit an operator to perform these actions. (H.2(c))  
The inspectors determined that this finding had a cross-cutting aspect in the area of human performance because Entergy did not ensure that complete, accurate and up-to-date procedures were available. Specifically, Entergy did not ensure that the venting procedure for the SI system had adequate guidance to ensure the SI system remained operable by controlling valve positions, or having detailed instructions to credit an operator to perform these actions. (H.2(c))  


=====Enforcement:=====
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures and Drawings," requires, in part, that activities affecting quality be prescribed by documented instructions or procedures of a type appropriate to the circumstances and include appropriate quantitative or qualitative acceptance criteria to determine that the activities were satisfactorily accomplished. Contrary to this, Entergy's procedure for venting SI pumps and piping contained in 2-PT-M108, "RHR/SI System Venting," did not contain instructions appropriate to the circumstances which would have ensured that the action was satisfactorily accomplished. Specifically, the procedure did not provide appropriate controls to ensure the SI piping and pumps remained operable during accident conditions. Because of the very low safety significance of this finding and because the finding was entered into Entergy's corrective action program as CR-IP2-2007-03032, 12this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000247/2007004-03, Procedure Inadequate to Ensure Operability of SI Pumps During Venting.
10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, requires, in part, that activities affecting quality be prescribed by documented instructions or procedures of a type appropriate to the circumstances and include appropriate quantitative or qualitative acceptance criteria to determine that the activities were satisfactorily accomplished. Contrary to this, Entergys procedure for venting SI pumps and piping contained in 2-PT-M108, RHR/SI System Venting, did not contain instructions appropriate to the circumstances which would have ensured that the action was satisfactorily accomplished. Specifically, the procedure did not provide appropriate controls to ensure the SI piping and pumps remained operable during accident conditions. Because of the very low safety significance of this finding and because the finding was entered into Entergys corrective action program as CR-IP2-2007-03032, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000247/2007004-03, Procedure Inadequate to Ensure Operability of SI Pumps During Venting.


===Cornerstone:===
===Cornerstone: Emergency Preparedness===
Emergency Preparedness 1EP2 Alert and Notification System Evaluation (71114.02 - 1 Sample)
1EP2 Alert and Notification System Evaluation (71114.02 - 1 Sample)


====a. Inspection Scope====
====a. Inspection Scope====
A region-based specialist inspector reviewed Entergy's activities related to the existing Indian Point alert and notification system (ANS), and reviewed the progress made in the design and installation of a new siren system. This inspection was conducted in accordance with the baseline inspection program deviation authorized by the NRC Executive Director of Operations (EDO) in a memorandum dated October 31, 2005, and renewed by the EDO in a memorandum dated December 11, 2006.
A region-based specialist inspector reviewed Entergys activities related to the existing Indian Point alert and notification system (ANS), and reviewed the progress made in the design and installation of a new siren system. This inspection was conducted in accordance with the baseline inspection program deviation authorized by the NRC Executive Director of Operations (EDO) in a memorandum dated October 31, 2005, and renewed by the EDO in a memorandum dated December 11, 2006.


The new siren system is being installed around the Indian Point Energy Center to satisfy commitments documented in an NRC Confirmatory Order (dated January 31, 2006) that implements the requirements outlined in the 2005 Energy Policy Act. In January 2007, Entergy requested an extension of the deadline for completing the ANS project as described in the Confirmatory Order. The Confirmatory Order set a January 30, 2007, deadline for completing installation. Entergy's extension request cited several issues that were beyond their control, as the basis for the delay. On January 23, 2007, the NRC granted Entergy's extension request and established April 15, 2007, as the new installation completion date. The licensee conducted a full-system demonstration test of the new ANS on April 12, and the results of that test failed to meet the acceptance criteria for the new system. On April 13, 2007, Entergy requested another extension which was subsequently denied. On April 23, 2007, the NRC issued a Notice of Violation (NOV) and civil penalty for Entergy's failure to comply with the siren operability date in the Confirmatory Order. On May 23, 2007, Entergy responded to the NOV and committed to August 24, 2007, as the latest date anticipated for declaring the new ANS operable.
The new siren system is being installed around the Indian Point Energy Center to satisfy commitments documented in an NRC Confirmatory Order (dated January 31, 2006) that implements the requirements outlined in the 2005 Energy Policy Act. In January 2007, Entergy requested an extension of the deadline for completing the ANS project as described in the Confirmatory Order. The Confirmatory Order set a January 30, 2007, deadline for completing installation. Entergys extension request cited several issues that were beyond their control, as the basis for the delay. On January 23, 2007, the NRC granted Entergys extension request and established April 15, 2007, as the new installation completion date. The licensee conducted a full-system demonstration test of the new ANS on April 12, and the results of that test failed to meet the acceptance criteria for the new system. On April 13, 2007, Entergy requested another extension which was subsequently denied. On April 23, 2007, the NRC issued a Notice of Violation (NOV) and civil penalty for Entergys failure to comply with the siren operability date in the Confirmatory Order. On May 23, 2007, Entergy responded to the NOV and committed to August 24, 2007, as the latest date anticipated for declaring the new ANS operable.


On August 30, the NRC issued a NOV to Entergy due to its failure to take timely and necessary actions to ensure the Federal Emergency Management Agency's (FEMA)approval for the use of the ANS by August 24, 2007. On September 12, 2007, FEMA issued a letter indicating that the new ANS was not adequate in the areas of acoustics, sound blockage from foliage, and control systems. In a letter dated September 21 2007, Entergy requested a meeting with FEMA to discuss the technical aspects of Entergy's proposed plans and determine a mutually acceptable schedule for resolving the open items.
On August 30, the NRC issued a NOV to Entergy due to its failure to take timely and necessary actions to ensure the Federal Emergency Management Agencys (FEMA)approval for the use of the ANS by August 24, 2007. On September 12, 2007, FEMA issued a letter indicating that the new ANS was not adequate in the areas of acoustics, sound blockage from foliage, and control systems. In a letter dated September 21 2007, Entergy requested a meeting with FEMA to discuss the technical aspects of Entergys proposed plans and determine a mutually acceptable schedule for resolving the open items.


The inspectors conducted the following onsite inspection activities during this quarter:
The inspectors conducted the following onsite inspection activities during this quarter:
* Observed the full-volume sounding to obtain far-field acoustical data (August 9, 2007); and 13
* Observed the full-volume sounding to obtain far-field acoustical data (August 9, 2007); and
* Met with Entergy representatives to discuss and obtain complete back-up battery testing results (August 13 - 14, 2007).
* Met with Entergy representatives to discuss and obtain complete back-up battery testing results (August 13 - 14, 2007).


Line 349: Line 366:


==RADIATION SAFETY==
==RADIATION SAFETY==
 
===Cornerstone: Occupational Radiation Safety (OS)===
===Cornerstone:===
2OS1 Access Control to Radiologically Significant Areas (71121.01 - 14 samples)
Occupational Radiation Safety (OS)2OS1 Access Control to Radiologically Significant Areas (71121.01 - 14 samples)


====a. Inspection Scope====
====a. Inspection Scope====
During July 16 through 19, 2007, the inspectors conducted the following activities to verify that the licensee was properly implementing physical, engineering, and administrative controls for access to high radiation areas, and other radiologically controlled areas, and that workers were adhering to these controls when working in these areas. Implementation of the access control program was reviewed against the criteria contained in 10 CFR 20, Technical Specifications, and the licensee's procedures.
During July 16 through 19, 2007, the inspectors conducted the following activities to verify that the licensee was properly implementing physical, engineering, and administrative controls for access to high radiation areas, and other radiologically controlled areas, and that workers were adhering to these controls when working in these areas. Implementation of the access control program was reviewed against the criteria contained in 10 CFR 20, Technical Specifications, and the licensees procedures.
: (1) There were no occupational exposure cornerstone performance indicator incidents during the current assessment period.
: (1) There were no occupational exposure cornerstone performance indicator incidents during the current assessment period.
: (2) The inspectors walked down exposure significant work areas of the plant (both Units 2 and 3) and reviewed licensee controls and surveys to determine if licensee surveys, postings, and barricades were acceptable and in accordance with regulatory requirements.
: (2) The inspectors walked down exposure significant work areas of the plant (both Units 2 and 3) and reviewed licensee controls and surveys to determine if licensee surveys, postings, and barricades were acceptable and in accordance with regulatory requirements.
: (3) The inspectors walked down exposure significant work areas of the plant (both Units 2 and 3) and conducted independent surveys to determine whether prescribed radiation work permit and procedural controls were in place and whether licensee surveys and postings were complete and accurate.
: (3) The inspectors walked down exposure significant work areas of the plant (both Units 2 and 3) and conducted independent surveys to determine whether prescribed radiation work permit and procedural controls were in place and whether licensee surveys and postings were complete and accurate.
: (4) There were no internal dose assessments greater than 50 mrem during 2007.
: (4) There were no internal dose assessments greater than 50 mrem during 2007.
: (5) The licensee's physical and programmatic controls for highly activated materials stored underwater in the Unit 2 and Unit 3 spent fuel pools were reviewed and 14evaluated through observation and a review of the applicable access control procedure.
: (5) The licensees physical and programmatic controls for highly activated materials stored underwater in the Unit 2 and Unit 3 spent fuel pools were reviewed and evaluated through observation and a review of the applicable access control procedure.
: (6) A review of licensee radiation protection program self-assessments and audits during 2007 was conducted to determine if identified problems were entered into the corrective action program for resolution.
: (6) A review of licensee radiation protection program self-assessments and audits during 2007 was conducted to determine if identified problems were entered into the corrective action program for resolution.
: (7) Seven condition reports associated with the radiation protection access control and ALARA areas between March 2007 and July 2007, were reviewed and discussed with licensee staff to determine if the follow-up activities were being conducted in an effective and timely manner commensurate with their safety significance.
: (7) Seven condition reports associated with the radiation protection access control and ALARA areas between March 2007 and July 2007, were reviewed and discussed with licensee staff to determine if the follow-up activities were being conducted in an effective and timely manner commensurate with their safety significance.
: (8) Based on the condition reports reviewed, repetitive deficiencies were screened to determine if the licensee's self-assessment activities were identifying and addressing these deficiencies.
: (8) Based on the condition reports reviewed, repetitive deficiencies were screened to determine if the licensees self-assessment activities were identifying and addressing these deficiencies.
: (9) There were no Occupational Exposure Performance Indicator incidents reported during the current assessment period.
: (9) There were no Occupational Exposure Performance Indicator incidents reported during the current assessment period.
: (10) Changes to the high radiation area and very high radiation area procedures since the last inspection in this area were reviewed and management of these changes were discussed with the Radiation Protection Manager.
: (10) Changes to the high radiation area and very high radiation area procedures since the last inspection in this area were reviewed and management of these changes were discussed with the Radiation Protection Manager.
: (11) Controls associated with potential changing plant conditions to anticipate timely posting and controls of radiation hazards was discussed with a radiation protection supervisor.
: (11) Controls associated with potential changing plant conditions to anticipate timely posting and controls of radiation hazards was discussed with a radiation protection supervisor.
: (12) All accessible locked high radiation area entrances in both Units 2 and 3 were verified to be locked through challenging the locks or doors.
: (12) All accessible locked high radiation area entrances in both Units 2 and 3 were verified to be locked through challenging the locks or doors.
: (13) Several radiological condition reports were reviewed to evaluate if the incidents were caused by radiation worker errors and determine if there were any trends or patterns and if the licensee's corrective actions were adequately addressing these trends.
: (13) Several radiological condition reports were reviewed to evaluate if the incidents were caused by radiation worker errors and determine if there were any trends or patterns and if the licensees corrective actions were adequately addressing these trends.
: (14) Several radiological condition reports were reviewed to evaluate if the incidents were caused by radiation protection technician errors and determine if there were any trends or patterns and if the licensee's corrective actions were adequately addressing these trends.
: (14) Several radiological condition reports were reviewed to evaluate if the incidents were caused by radiation protection technician errors and determine if there were any trends or patterns and if the licensees corrective actions were adequately addressing these trends.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
 
2OS2 ALARA Planning and Controls (71121.02 - 2 samples)
15 2OS2 ALARA Planning and Controls (71121.02 - 2 samples)


====a. Inspection Scope====
====a. Inspection Scope====
During July 16 through 19, 2007, the inspectors conducted the following activities to verify that the licensee was properly maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). Implementation of the ALARA program was reviewed against the criteria contained in 10 CFR 20.1101(b) and the licensee's procedures.
During July 16 through 19, 2007, the inspectors conducted the following activities to verify that the licensee was properly maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). Implementation of the ALARA program was reviewed against the criteria contained in 10 CFR 20.1101(b) and the licensees procedures.
: (1) The procedure and methodology for adjusting work activity exposure estimates was evaluated to include revisions for emergent work and unexpected radiological conditions. The methodology for the exposure estimate adjustments was evaluated with respect to sound radiation protection and ALARA principles and to ensure the revised exposure estimates provided an effective ALARA performance measure.
: (1) The procedure and methodology for adjusting work activity exposure estimates was evaluated to include revisions for emergent work and unexpected radiological conditions. The methodology for the exposure estimate adjustments was evaluated with respect to sound radiation protection and ALARA principles and to ensure the revised exposure estimates provided an effective ALARA performance measure.
: (2) Based on the condition reports reviewed, repetitive deficiencies in the ALARA program were screened to determine if the licensee's self-assessment activities were identifying and addressing these deficiencies.
: (2) Based on the condition reports reviewed, repetitive deficiencies in the ALARA program were screened to determine if the licensees self-assessment activities were identifying and addressing these deficiencies.


====b. Findings====
====b. Findings====
Line 384: Line 399:


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
[OA]
[OA]  
{{a|4OA1}}


{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151|count=3}}
{{IP sample|IP=IP 71151|count=3}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed performance indicator (PI) data for the cornerstones listed below and used Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, to verify individual PI accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment.
The inspectors reviewed performance indicator (PI) data for the cornerstones listed below and used Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, to verify individual PI accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment.


Mitigating Systems Cornerstone
Mitigating Systems Cornerstone
Line 398: Line 413:


Barrier Integrity Cornerstone
Barrier Integrity Cornerstone
* Reactor Coolant System Leakage (January 2006 - June 2007)16The inspectors reviewed data and plant records from the above noted periods. The records included PI data summary reports, licensee event reports, operator narrative logs, the licensee corrective action program, and Maintenance Rule records. The inspectors verified the accuracy of the number of critical hours reported, and interviewed the system engineers and operators responsible for data collection and evaluation.
* Reactor Coolant System Leakage (January 2006 - June 2007)
The inspectors reviewed data and plant records from the above noted periods. The records included PI data summary reports, licensee event reports, operator narrative logs, the licensee corrective action program, and Maintenance Rule records. The inspectors verified the accuracy of the number of critical hours reported, and interviewed the system engineers and operators responsible for data collection and evaluation.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|4OA2}}
{{a|4OA2}}
 
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
===.1 Routine Problem Identification and Resolution (PI&R) Program Review===
===.1 Routine Problem Identification and Resolution (PI&R) Program Review===
====a. Inspection Scope====
====a. Inspection Scope====
As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergys corrective action program. The review was accomplished by accessing Entergys computerized database for condition reports (CRs) and attending CR screening meetings.
and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergy's corrective action program. The review was accomplished by accessing Entergy's computerized database for condition reports (CRs) and attending CR screening meetings.


In accordance with the baseline inspection modules, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for additional follow-up and review. The inspectors assessed Entergy's threshold for problem identification, the adequacy of the cause analyses, extent of condition reviews, operability determinations, and the timeliness of the specified corrective actions. The CRs reviewed during this inspection are listed in the Attachment.
In accordance with the baseline inspection modules, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for additional follow-up and review. The inspectors assessed Entergys threshold for problem identification, the adequacy of the cause analyses, extent of condition reviews, operability determinations, and the timeliness of the specified corrective actions. The CRs reviewed during this inspection are listed in the Attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


{{a|4OA3}}
{{a|4OA3}}
 
==4OA3 Event Followup==
==4OA3 Event Followup==
{{IP sample|IP=IP 71153|count=1}}
{{IP sample|IP=IP 71153|count=1}}


===.1 Operations performance during single control rod drop of 20 steps on August 23, 2007===
===.1 Operations performance during single control rod drop of 20 steps on August 23, 2007===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed control room personnel response during an unexpected control rod drop on August 23, 2007, that occurred during control rod surveillance testing. During control rod exercise testing of Shutdown Bank 'B,' control rod G-3 dropped from 213 steps to 198 steps with no operator action. The inspectors observed Entergy's response in the control room to verify that plant equipment response was appropriately evaluated, and to ensure that operating procedures were being appropriately implemented. The inspectors discussed the event and corrective actions with plant management in order to confirm that 17Entergy had taken appropriate corrective actions in restoring the plant. The documents reviewed are included in the Attachment.
The inspectors observed control room personnel response during an unexpected control rod drop on August 23, 2007, that occurred during control rod surveillance testing. During control rod exercise testing of Shutdown Bank B, control rod G-3 dropped from 213 steps to 198 steps with no operator action. The inspectors observed Entergys response in the control room to verify that plant equipment response was appropriately evaluated, and to ensure that operating procedures were being appropriately implemented. The inspectors discussed the event and corrective actions with plant management in order to confirm that Entergy had taken appropriate corrective actions in restoring the plant. The documents reviewed are included in the Attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|4OA5}}
{{a|4OA5}}
 
==4OA5 Other Activities==
==4OA5 Other Activities==
===.1 Groundwater Contamination Investigation===
===.1 Groundwater Contamination Investigation===
====a. Inspection Scope====
====a. Inspection Scope====
Continued inspection of Entergy's plans, procedures, and characterization activities affecting the contaminated groundwater condition at Indian Point, relative to NRC regulatory requirements, was authorized by the NRC Executive Director of Operations in a Reactor Oversight Process deviation memorandum dated October 31, 2005 (ADAMS Accession Number ML053010404) and renewed on December 11, 2006 (ADAMS Accession Number ML063480016). Accordingly, continuing oversight of licensee progress has been conducted throughout this quarterly inspection report period, which included: onsite review of licensee performance, progress, and achievements; independent split sample analyses of selected monitoring wells; expanded sampling of the edible portions of various fish collected from multiple locations in the Hudson River; review of an onsite underground auxiliary steam pipe leak; and frequent communication of NRC observations with interested Federal, State, and local government stakeholders.
Continued inspection of Entergys plans, procedures, and characterization activities affecting the contaminated groundwater condition at Indian Point, relative to NRC regulatory requirements, was authorized by the NRC Executive Director of Operations in a Reactor Oversight Process deviation memorandum dated October 31, 2005 (ADAMS Accession Number ML053010404) and renewed on December 11, 2006 (ADAMS Accession Number ML063480016). Accordingly, continuing oversight of licensee progress has been conducted throughout this quarterly inspection report period, which included: onsite review of licensee performance, progress, and achievements; independent split sample analyses of selected monitoring wells; expanded sampling of the edible portions of various fish collected from multiple locations in the Hudson River; review of an onsite underground auxiliary steam pipe leak; and frequent communication of NRC observations with interested Federal, State, and local government stakeholders.


In July and August 2007, NRC staff and U.S. Geological Survey (USGS) scientists, in consultation with representatives of New York State Department of Environmental Conservation, conducted an independent assessment of selected data and information developed by Entergy and its geophysical contractor relative to fracture flow modeling, and groundwater characterization relative to flow and transport.
In July and August 2007, NRC staff and U.S. Geological Survey (USGS) scientists, in consultation with representatives of New York State Department of Environmental Conservation, conducted an independent assessment of selected data and information developed by Entergy and its geophysical contractor relative to fracture flow modeling, and groundwater characterization relative to flow and transport.


The methodology applied by USGS utilized data collected from downhole geophysical and flow logs conducted by Geophysical Applications, Inc, under the direction of the Entergy's principal contractor for the groundwater investigations, GeoEnvironmental, Inc. (GZA).
The methodology applied by USGS utilized data collected from downhole geophysical and flow logs conducted by Geophysical Applications, Inc, under the direction of the Entergys principal contractor for the groundwater investigations, GeoEnvironmental, Inc. (GZA).


The geophysical data (i.e., caliper, optical and acoustic televiewer, fluid resistivity and temperature logs), fracture mapping and flow logs were processed and visualized with a computer-based system, WELLCAD. The method permitted a systematic mapping of fracture orientations, density, associated flow conditions and properties using composite portrayals of vertical plots of the geophysical logs and hydraulic test data and analyses.
The geophysical data (i.e., caliper, optical and acoustic televiewer, fluid resistivity and temperature logs), fracture mapping and flow logs were processed and visualized with a computer-based system, WELLCAD. The method permitted a systematic mapping of fracture orientations, density, associated flow conditions and properties using composite portrayals of vertical plots of the geophysical logs and hydraulic test data and analyses.


These composite portrayals facilitated comparisons and analyses of selected IPEC monitoring wells for the determination of the location and direction of discrete high flow zones, including associated flux and transmissivity. It is expected that the information and analyses will aid the NRC and USGS staff in evaluations of GZA's conceptual groundwater flow and transport model that was derived from previous hydraulic pump and tracer tests conducted on selected monitoring wells.
These composite portrayals facilitated comparisons and analyses of selected IPEC monitoring wells for the determination of the location and direction of discrete high flow zones, including associated flux and transmissivity. It is expected that the information and analyses will aid the NRC and USGS staff in evaluations of GZAs conceptual groundwater flow and transport model that was derived from previous hydraulic pump and tracer tests conducted on selected monitoring wells.


====b. Findings and Observations====
====b. Findings and Observations====
No findings of significance were identified.
No findings of significance were identified.


The fracture flow assessment provided an effective means of visualizing fracture zones and properties of certain IPEC monitoring wells; and provided an enhanced conceptualization of groundwater flow and transport characteristics which is important to the NRC's overall assessment of the licensee's groundwater modeling and characterization. The NRC and USGS will apply the knowledge gained from this assessment for independent review of Entergy's characterization of groundwater behavior, its selection of monitoring locations and performance indicators for long-term site groundwater monitoring, and its determination of remediation strategies, as appropriate. This assessment provides another tool to be used to effectively verify and validate that Entergy's groundwater modeling and dose assessment methods continue to assure that public health and safety, and protection of the environment is maintained.
The fracture flow assessment provided an effective means of visualizing fracture zones and properties of certain IPEC monitoring wells; and provided an enhanced conceptualization of groundwater flow and transport characteristics which is important to the NRCs overall assessment of the licensees groundwater modeling and characterization. The NRC and USGS will apply the knowledge gained from this assessment for independent review of Entergys characterization of groundwater behavior, its selection of monitoring locations and performance indicators for long-term site groundwater monitoring, and its determination of remediation strategies, as appropriate. This assessment provides another tool to be used to effectively verify and validate that Entergys groundwater modeling and dose assessment methods continue to assure that public health and safety, and protection of the environment is maintained.


During this period, the NRC continued split sampling of selected monitoring wells for independent analysis by the Oak Ridge Institute for Science and Education, Environmental Site Survey and Assessment Program (ORISE/ESSAP) radioanalytical laboratory. The NRC's assessment of the licensee's sample analytical results data indicated that the licensee's analytical contractor reported final sample results that were comparable with the NRC's analytical results.
During this period, the NRC continued split sampling of selected monitoring wells for independent analysis by the Oak Ridge Institute for Science and Education, Environmental Site Survey and Assessment Program (ORISE/ESSAP) radioanalytical laboratory. The NRCs assessment of the licensees sample analytical results data indicated that the licensees analytical contractor reported final sample results that were comparable with the NRCs analytical results.


Fish samples were also split and independently analyzed during this period. The samples were collected from three separate locations on the Hudson River (i.e., an area in the near vicinity of the plant, the Roseton control location (20-30 miles, up river), and the Catskills region (about 80 to 90 miles, up river)). The NRC analyzed edible portions of the fish samples, commensurate with the requirements of the environmental monitoring program and the existing pathway for exposure from liquid radiological releases to the Hudson River. None of the 18 samples indicated any detectable radioactivity distinguishable from background (i.e., all samples were less than the Minimum Detectable Activity established by ORISE for gamma and strontium-90 radionuclides).
Fish samples were also split and independently analyzed during this period. The samples were collected from three separate locations on the Hudson River (i.e., an area in the near vicinity of the plant, the Roseton control location (20-30 miles, up river), and the Catskills region (about 80 to 90 miles, up river)). The NRC analyzed edible portions of the fish samples, commensurate with the requirements of the environmental monitoring program and the existing pathway for exposure from liquid radiological releases to the Hudson River. None of the 18 samples indicated any detectable radioactivity distinguishable from background (i.e., all samples were less than the Minimum Detectable Activity established by ORISE for gamma and strontium-90 radionuclides).


The NRC's ORISE/ESSAP sample results are available in ADAMS under the following Accession Numbers: ML072840255, ML072840278, ML072840292, ML072840312, ML072840323, ML072840334, ML072840357. To date, plant-related radioactivity has not been detected in any of the site's southern boundary wells or offsite environmental groundwater monitoring locations. Information collected and assessed to-date, continues to support that the estimated radiological release fraction through groundwater is negligible relative to NRC regulatory limits.
The NRCs ORISE/ESSAP sample results are available in ADAMS under the following Accession Numbers: ML072840255, ML072840278, ML072840292, ML072840312, ML072840323, ML072840334, ML072840357. To date, plant-related radioactivity has not been detected in any of the sites southern boundary wells or offsite environmental groundwater monitoring locations. Information collected and assessed to-date, continues to support that the estimated radiological release fraction through groundwater is negligible relative to NRC regulatory limits.


On April 7, 2007, two separate underground steam leaks were detected emanating through the asphalt surfaces west and north of Unit 3. The affected 8" auxiliary steam line was isolated on April 23, 2007, and subsequently excavated and replaced. As expected, a very low tritium concentration was detected in the area, likely due to normal tritium diffusion or deposition onsite, Condition Report No. CR-IP3-2007-1852 pertains. Entergy performed a very conservative bounding evaluation of the resulting ground and air 19releases that indicated approximately 1E-8 mrem/yr and 2E-6 mrem/yr due to the liquid and air release pathways, respectively. Such releases are not considered significant and are below reporting requirements.
On April 7, 2007, two separate underground steam leaks were detected emanating through the asphalt surfaces west and north of Unit 3. The affected 8" auxiliary steam line was isolated on April 23, 2007, and subsequently excavated and replaced. As expected, a very low tritium concentration was detected in the area, likely due to normal tritium diffusion or deposition onsite, Condition Report No. CR-IP3-2007-1852 pertains. Entergy performed a very conservative bounding evaluation of the resulting ground and air releases that indicated approximately 1E-8 mrem/yr and 2E-6 mrem/yr due to the liquid and air release pathways, respectively. Such releases are not considered significant and are below reporting requirements.


{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings, including Exit==
==4OA6 Meetings, including Exit==
===Exit Meeting Summary===
===Exit Meeting Summary===
On October 3, 2007, the inspectors presented the inspection results to Mr. Anthony Vitale and other Entergy staff members, who acknowledged the inspection results presented.
On October 3, 2007, the inspectors presented the inspection results to Mr. Anthony Vitale and other Entergy staff members, who acknowledged the inspection results presented.


Entergy did not identify any material as proprietary.
Entergy did not identify any material as proprietary.


ATTACHMENT:
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
 
Entergy Personnel  
Entergy Personnel
: [[contact::B. Christman]], Manager of Training and Development  
: [[contact::B. Christman]], Manager of Training and Development  
: [[contact::P. Conroy]], Director of Nuclear Safety Assurance  
: [[contact::P. Conroy]], Director of Nuclear Safety Assurance  
Line 479: Line 490:
: [[contact::S. Manzione]], Component Engineering Supervisor  
: [[contact::S. Manzione]], Component Engineering Supervisor  
: [[contact::B. McCarthy]], Indian Point Unit 2 Assistant Operations Manager  
: [[contact::B. McCarthy]], Indian Point Unit 2 Assistant Operations Manager  
: [[contact::E. O'Donnell]], Indian Point Unit 2 Operations Manager  
: [[contact::E. ODonnell]], Indian Point Unit 2 Operations Manager  
: [[contact::T. Orlando]], Director of Engineering  
: [[contact::T. Orlando]], Director of Engineering  
: [[contact::D. Parker]], Maintenance Superintendent  
: [[contact::D. Parker]], Maintenance Superintendent  
Line 491: Line 502:


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
===Opened and Closed===
===Opened and Closed===
: 05000247/2007004-01 NCV  Degraded 12 Fire Main Booster Pump Cell Fire Door. (Section 1R05)
: 05000247/2007004-01  
: 05000247/2007004-02  NCV  Untimely Corrective Actions to Repair a Degraded Service Water Flow Instrument. 
(Section 1R13)
: 05000247/2007004-03  NCV  Procedure Inadequate to Ensure Operability of SI Pumps During Venting.  (Section 1R22)


==LIST OF DOCUMENTS REVIEWED==
NCV
==Section 1R01: Adverse Weather Protection==


===Procedures===
Degraded 12 Fire Main Booster Pump Cell Fire Door. (Section 1R05)
: OAP-008, "Severe Weather Preparations," Revision 1
: 05000247/2007004-02  
: SOP 24.1.1, "Hot Weather Preparations," Revision 9
: 3PT-Q101, main Steam valves Stroke test, revision 11
: IP-SMM-OP-104, "Offsite Power Continuous Monitoring and Notification," Revision 6
: ECA 0.0, Loss of All AC, Revision 41
: ECA 0.0, Loss of All AC, Revision 0 
===Miscellaneous===
: IPEC Letter
: NL-06-043, Entergy Northeast Response to Generic Letter 2006-02, Grid Reliability and The Impact on Plant Risk and Operability of Offsite Power, April 3, 2006
: Transaction Form, Con Edison and Entergy Nuclear Operations, June 7, 2006
: NYISO Major Emergency Report, August 4, 2007
: PQE-20.1, EQ file Installed transmitter 1153HD4PB, Revision 1
: Report
: IP-RPT-04-00337, Station Blackout report Final, March 9, 1990 
===Condition Reports===
: IP2-2007-03284
: IP2-2007-03353 
===Calculations===
: IP-CALC-07-00143, Auxiliary FeedWater Pump Room temperatures, Revision 6


==Section 1R04: Equipment Alignment==
NCV


===Procedures===
Untimely Corrective Actions to Repair a Degraded Service Water Flow Instrument.  
: 2-SOP-27.3.1.1, "21 Emergency Diesel Generator Manual Operation," Revision 16
(Section 1R13)
: 2-SOP-27.3.1.3, "23 Emergency Diesel Generator Manual Operation," Revision 16
: 05000247/2007004-03
: 2-PT-M021B, "Emergency Diesel Generator 23 Load Test," Revision 14
: 2-COL-27.3.1, "Diesel Generators," Revision 25
: 2-PT-M048, "480 Volt Undervoltage Alarm," Revision 20
: 2-COL-24.1.1, "Service Water and Closed Cooling Water Systems," Revision 41
: PT-M34A, "11 Fire Main Booster Pump," Revision 1
: 2-COL-29.6, "Fire Protection System," Revision 54 
===Drawings===
: 9321-H-2029, "Flow Diagram, Starting Air to Diesel Generators" 
: 21-F-2030, "Flow Diagram, Fuel Oil to Diesel Generators"
: A207698, "Flow Diagram, Lube Oil for Diesel generators No. 21, 22 & 23"
: A227552, "Fire Protection System Diagram, Sheet 2"
: A227553, "Fire Protection System Diagram, Sheet 3"


==Section 1R05: Fire Protection==
NCV


===Procedures===
Procedure Inadequate to Ensure Operability of SI Pumps During Venting. (Section 1R22)
: ENN-DC-161, "Transient Combustible Program," Revision 1
: ENN-DC-189, "Fire Drills," Revision 0
: SAO-703, "Fire Protection Impairment Criteria and Surveillance," Revision 25
: PT-M55, "Fire Doors," Revision 12
: 2-PT-SA020, "Swing Fire Doors," Revision 0 
===Condition Reports===
: IP2-2006-06613
: IP2-2007-01670
: IP2-2007-02393
: IP2-2007-03562
: IP2-2007-03561
: IP2-2006-00945
: IP2-2006-02072
: IP2-2006-02203
: IP2-2006-04242
: IP2-2007-00389
: IP2-2007-03651
: IP2-2007-00318 
===Work Orders===
: IP2-06-01177
: IP2-06-27924 
===Miscellaneous===
: Indian Point Nuclear Generating Station, Unit No. 2, "Fire Protection Program Plan," Revision 9
: IP2-RPT-03-00015, "IP2 Fire Hazards Analysis," Revision 3


==Section 1R06: Flood Protection Measures==
==LIST OF DOCUMENTS REVIEWED==
 
===Condition Reports===
: IP-2-2007-03035 
===Miscellaneous===
: USNRC Safety Evaluation report (SER), Susceptibility of Safety Related Systems to Flooding  from failure of Non-Category I systems for Indian Point Unit 2, November 1980 ANSI 18.2- 1975, Revision and Addendum to Nuclear Safety Criteria for the Design of Stationary Pressurized Water Reactor Plants
 
==Section 1R11: Licensed Operator Requalification Program==
 
===Procedures===
: 2-FR-C.2, "Response to Degraded Core Cooling," Revision 0 2-E-0, "Reactor Trip or Safety Injection," Revision 0 2-E-1, "Loss of Reactor or Secondary Coolant," Revision 0
: 2-AOP-LEAK-1, "Sudden Increase in Reactor Coolant System Leakage," Revision 7
: 2-AOP-INST-1, "Instrument/Controller Failures," Revision 4 
===Miscellaneous===
: IPEC Simulator Guide, Lesson Plan
: SES-FR-C.2, Revision 2
: A-4
 
==Section 1R12: Maintenance Effectiveness==
 
===Condition Reports===
: IP2-2006-01426
: IP2-2006-01883
: IP2-2006-02133
: IP2-2006-02156
: IP2-2004-06143
: IP2-2006-03094
: IP2-2006-03958
: IP2-2006-04438
: IP2-2006-05427
: IP2-2006-07092
: IP2-2007-02514
: IP2-2007-02665
: IP2-2007-03226
: IP2-2007-03701
: IP2-2007-03820
: IP2-2007-03822
: IP2-2006-06499
: IP2-2007-00472 
===Procedures===
: EN-DC-203, "Maintenance Rule Program," Revision 0
: EN-DC-204, "Maintenance Scope and Basis," Revision 0
: EN-DC-205, "Maintenance Rule Monitoring," Revision 0
: EN-DC-324, "Preventive Maintenance Process," Revision 3
: EN-LI-102, "Corrective Action Process," Revision 10
: SEP-SW-001, "Generic Letter 89-13 Service Water Program," Rev 1 
===Drawings===
: A209762, "Flow Diagram, Service Water System (Sh 2 of 2)"
: 21-F-2722-117, Flow Diagram, Service Water System (Sh 1 of 2)" 
===Work Orders===
: IP2-03-03082
: IP2-06-17587
: IP2-06-17592
: IP2-06-22281
: IP2-06-24701
: IP2-06-00839
: IP2-07-19751
: 51320679
: 287133
: IP2-07-00578
: IP2-07-20411
: 00105027
: 00107732
: 00123831
: 00108250
: IP2-04-33407 
===Miscellaneous===
: IP2 Service Water System Health Report, 2
nd Quarter 2007 IP2 SW Pipe Inspection NDE Checklist, 2R16 (10/2004)
: IP2 SW Pipe Inspection NDE Checklist, 2R17 (4/2006)
: IPEC Maintenance Rule Basis Document, Service Water (SW) - Rev 0
 
==Section 1R13: Maintenance Risk Assessments and Emergent Work Control==
 
===Procedures===
: IP-SMM-OP-104, "Offsite Power Continuous Monitoring and Notification," Revision 6
: IP-SMM-WM-101, "On-Line Risk Assessment," Revision 2
: EN-MA-125, "Troubleshooting Control of Maintenance Activities," Revision 3
: OAP-030, "Infrequently Performed Tests and Evolutions," Revision 1 
===Condition Reports===
: IP2-2007-03067
: IP2-2006-04779
: IP2-2006-04792
: IP2-2006-05577
: IP2-2006-06735
: IP2-2006-07115
: IP2-2006-07117
: IP2-2006-07329
: IP2-2007-01627
: IP2-2007-01712
: IP2-2007-01721
: IP2-2007-01840
: IP2-2006-04946
: IP2-2006-05373
: IP2-2006-05829
: IP2-2006-05972
: IP2-2006-06511
: IP2-2007-00124
: IP2-2007-01789
: IP2-2007-03421
: IP2-2007-03444
: IP2-2007-03536
: IP2-2007-03532
: IP2-2007-03535 
: A-5IP2-2007-03338 
===Work Orders===
: 00118741 
===Drawings===
: B225300, "Instrumentation Block Diagram," 
: B208052, "Wiring diagram of Engine Generator Set for Diesel Generators," Revision 9
: 21-LL-3133, "Schematic Diagram Generator Heaters," Revision 3
: A208508, "Wiring Diagram Diesel Generator 22," Revision 23
: S000285, "DC Schematic for Diesel Generator 22," Revision 14
===Miscellaneous===
: Risk assessment with 22 AFW pump OOS August 2, 2007
: Risk assessment with Rod Control in manual September 4, 2007
 
==Section 1R15: Operability Evaluations==
 
===Procedures===
: 2-PT-W010, Weekly Battery Surveillance requirement, performed August 8, 2007
: 2-PT-Q016, "Containment Fan Cooler Unit Cooling Water Flow Test," Revision 1 
===Condition Reports===
: IP2-2007-03161
: IP2-2007-06983
: IP2-2007-00138
: IP2-2007-03035
: IP2-2007-03263
: IP2-2007-03264
: IP2-2007-03226
: IP2-2007-02665
: IP2-2007-02514
: IP2-2006-01625
: IP2-2007-03275 
===Miscellaneous===
: Spec 9321-01-248-35, Section V, "Piping Schedule and Materials," Revision 6A
: IP2-CCF DBD, "Design Basis Document for Containment Cooling and Filtration System," Rev 1
: IP2-SW DBD, "Design Basis Document for Service Water System," Revision 1
: Ultrasonic test report
: IP2-UT-07-015, "Through Wall Leak on Tee Fitting Body Downstream of
: SWN-840" Ultrasonic test report
: IP2-UT-07-016, "New Through Wall Leak on Tee Fitting Body Downstream of
: SWN-840" Ultrasonic test report
: IP2-UT-07-017, "Follow-Up - Through Wall Leak on Tee Fitting Body Downstream of
: SWN-840" Ultrasonic test report
: IP2-UT-07-020, "Weld Overlay of Tee Fitting Downstream of
: SWN-840 After Welding Complete" IEEE
: STD 450-1995,Recommended Practice for Maintenance, testing and Replacement of
: Vented Lead Acid Batteries for Stationary Applications, 1995 
===Work Orders===
: IP2-2007-19753 
===Calculations===
: A-6IP3-CALC-SI-01374,
: SI-MOV-885A and 885B D/P calc., January 7, 1995
: MMS-00120,
: MOV-888A, September 30, 2004
: IP-CALC-07-00175, "Evaluation of through wall flaw at leak downstream of
: SWN-71-5B," Rev 0
: IP-CALC-07-00207, "Through Wall Leak Evaluation of Line 406 Up-Stream of Valve
: SWN-46,"
: Rev. 0
 
==Section 1R19: Post-Maintenance Testing==
 
===Condition Reports===
: IP2-2007-03172
: IP2-2007-03287
: IP2-2007-03448
: IP3-2007-03754
: IP2-2007-03755
: IP2-2007-03745
: IP2-2007-03770 
===Procedures===
: 2-PC-R21B-1, "Recirculation Sump Continuous Level Transmitters," Revision 7
: OAP-007, "Containment Entry and Egress," Revision 12
: 2-SOP-31.1.2, "Gas Turbine 1 Local Operations," Revision 26
: PT-M38A, "Gas Turbine No.1," Revision 5
: PT-A36A, "Gas Turbine #1 Overspeed," Revision 8
: 2-PT-Q033C, "23 Charging Pump," Revision 10
: 2-PT-Q68C, "23 Charging Pump Check Valves," Revision 3
: 2-PT-Q027B, "23 Auxiliary Feed Pump"
: EN-OP-102, "Protective and Caution Tagging," Revision 6
: OAP-024, "Operations Testing," Revision 3
: 2-PT-Q026D, "24 Service Water Pump," Revision 9
: 2-PT-Q033B, "22 Charging Pump," Revision 11
: 2-OSP-3.1, "Support Procedure - Charging Sealwater and Letdown Control," Revision 4
: BAT-C-001-A, "Replacement of Battery Cells," Revision 8
: 0-VLV-413-MOV, "Motor Operated Valve Preventive Maintenance," Revision 2
: 0-VLV-404-AOV, "Use of Air Operated Valve Diagnostics," Revision 3 
===Work Orders===
: 51322853 (01)
: IP2-02-01124
: IP2-04-13788
: IP2-06-28102
: IP2-07-20321
: IP2-05-28592
: IP2-07-19000
: IP2-07-12316
: IP2-07-00032
: 51314704 (01)
: 51314704 (02)
: IP2-06-26506
: 51317764 (01)
: 51317764 (02)
: IP2-06-30654
: IP2-06-30655
: IP2-06-00827
: IP2-07-14504
: 51314378
: IP2-06-25990
: IP2-06-25986
: IP2-05-00578 
===Drawings===
: 310438-8, "Containment Sump, Reactor Cavity Pit & Recirc Sump Level Instrumentation," Revision 8
 
==Section 1R22: Surveillance Testing==
 
===Condition Reports===
: IP2-2007-03032
: IP2-2006-06996
: IP2-2006-07258
: IP2-2006-01474
: IP2-2006-01025
: IP2-2006-03477
: IP2-2006-05294
: IP2-2006-05871
===Procedures===
: 2-PT-M7, "Analog Rod Position Functional," Revision 28
: 0-LUB-401-GEN, "Lubrication of Plant Equipment," Revision 5
: 0-OSP-TG-001, "Main Turbine Stop and Control Valve Contingency Actions," Revision 0
: 2-PT-Q27B, "23 Auxiliary Feedwater Pump," Revision 14
: 2-PT-SA67, "Main Turbine Stop and Control Valves Exercise Test," Revision 4
: 3-PT-Q120A, "31 ABFP (Motor-Driven) Surveillance and IST," Revision 10
: 2-SOP-21.3, "Auxiliary Feedwater System Operation," Revision 36
: PT-2Y11A, "Gas Turbine 1 Blackstart Timing," Revision 2
: 2-PT-Q029A, "21 Safety Injection Pump," Revision 18
: 2-PT-M108, RHR/SI System Venting,  revision 3
: 2-PT-Q034, 22 AFW Pump , revision 23 (performed August 3, 2007)
: 2-PT-Q016, "Containment Fan Cooler Unit Cooling Water Flow Test," Revision 1
: 0-SOP-LEAKRATE-001, "RCS Leakage Surveillance, Evaluation and Identification," Revision 0 
===Work Orders===
: IP2-06-01558
 
==Section 4OA1: Performance Indicator Verification==
 
===Procedures===
: EN-LI-114, "Performance Indicator Process," Revision 2
: NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5
: 2-PT-Q028A, "21 RHR Pump," Revision 18
: MSPI Basis Document, Revision 7 
===Condition Reports===
: IP2-2006-04338
: IP2-2006-04341 IP2-2006-07108
 
==Section 4OA2: Identification and Resolution of Problems==
 
===Procedures===
: EN-OP-104, "Operability Determinations," Revision 2
: OAP-045, "Operator Burden Program," Revision 0 and 1
 
==Section 4OA3: Event Followup==


===Procedures===
: 2-AOP-ROD-1, "Rod control Malfunctions" 
===Condition Report===
: IP2-2007-03001
: IP2-2007-00197
: A-8Miscellaneous Calculation
: FIX-00117, Containment temperature Loop Uncertainty, revision 1
: 2-PT-D001, Control Room Operations Surveillance Requirements, revision 14
==LIST OF ACRONYMS==
: [[ADAMS]] [[agency wide document and management system]]
: [[ALARA]] [[as low as reasonable achievable]]
: [[ANS]] [[alert and notification system]]
: [[BTR]] [[Branch Technical Position]]
: [[CAP]] [[corrective action program]]
: [[CFR]] [[Code of Federal Regulations]]
: [[CR]] [[condition report]]
: [[CRVS]] [[Control Room Ventilation System]]
: [[ECCS]] [[emergency core cooling system]]
: [[EDG]] [[emergency diesel generator]]
: [[EDO]] [[Executive Director for Operations]]
: [[ESSAP]] [[Environmental Site Survey and Assessment Program]]
: [[FCU]] [[fan cooler unit]]
FEMA  Federal Emergency Management Agency
°F  Fahrenheit
gpm  gallons per minute
: [[IMC]] [[Inspection Manual Chapter]]
: [[IPEC]] [[Indian Point Energy Center]]
: [[LER]] [[Licensee Event Report]]
: [[NCV]] [[non-cited violation]]
: [[NRC]] [[Nuclear Regulatory Commission]]
: [[ORISE]] [[Oak Ridge Institute for Science and Education]]
: [[PARS]] [[Publically Available Records System]]
: [[PI]] [[performance indicator]]
: [[PI&R]] [[problem identification and resolution]]
: [[RHR]] [[residual heat removal]]
: [[SDP]] [[significance determination process]]
: [[SI]] [[safety injection]]
: [[SSC]] [[structures, systems, or components]]
: [[TS]] [[Technical Specifications]]
: [[UFSAR]] [[Updated Final Safety Evaluation Report]]
: [[USGS]] [[]]
: [[U.S.]] [[Geological Survey]]
: [[WO]] [[work order]]
}}
}}

Latest revision as of 20:11, 14 January 2025

IR 05000247-07-004, on 07/01/2007 - 09/30/2007; Indian Point, Unit 2; Fire Protection, Maintenance Risk Assessment and Emergent Work Control, and Surveillance Testing
ML073170091
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 11/09/2007
From: Cobey E
Reactor Projects Branch 2
To: Dacimo F
Entergy Nuclear Operations
Cobey, Eugene W. RI/DRP/PB2/610-337-5171
References
FOIA/PA-2010-0209 IR-07-004
Download: ML073170091 (40)


Text

November 9, 2007

SUBJECT:

INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED INSPECTION REPORT 05000247/2007004

Dear Mr. Dacimo:

On September 30, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report documents the inspection results, which were discussed on October 3, 2007, with Mr. Anthony Vitale and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents three findings of very low safety significance (Green). These findings were also determined to be violations of NRC requirements. However, because of their very low safety significance, and because they were entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a written response within 30 days of the date of this inspection report with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington D.C. 220555-001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 2.

In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eugene W. Cobey, Chief Projects Branch 2 Division of Reactor Projects

Docket No. 50-247 License No. DPR-26

Enclosure: Inspection Report No. 05000247/2007004

w/ Attachment: Supplemental Information

cc w/encl:

J. Wayne Leonard, Chairman and CEO, Entergy Nuclear Operations, Inc.

G. J. Taylor, Chief Executive Officer, Entergy Operations M. Kansler, President & CEO/CNO, Entergy Nuclear Operations, Inc.

J. T. Herron, Senior Vice President, Entergy Nuclear Operations, Inc.

M. Balduzzi, Senior Vice President & COO, Regional Operations Northeast Senior Vice President of Engineering and Technical Services J. DeRoy, Vice President, Operations Support (ENO)

A. Vitale, General Manager, Plant Operations O. Limpias, Vice President, Engineering (ENO)

J. McCann, Director, Nuclear Safety and Licensing (ENO)

J. Lynch, Manager, Licensing (ENO)

E. Harkness Director of Oversight (ENO)

P. Conroy, Director, Nuclear Safety Assurance W. Dennis, Assistant General Counsel, Entergy Nuclear Operations, Inc.

P. Tanko, President and CEO, New York State Energy Research and Development Authority P. Eddy, Electric Division, New York State Department of Public Service P. Smith, President, NYS Energy, Research, and Development Authority C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law D. ONeill, Mayor, Village of Buchanan J. G. Testa, Mayor, City of Peekskill R. Albanese, Four County Coordinator S. Lousteau, Treasury Department, Entergy Services, Inc.

Chairman, Standing Committee on Energy, NYS Assembly Chairman, Standing Committee on Environmental Conservation, NYS Assembly Chairman, Committee on Corporations, Authorities, and Commissions M. Slobodien, Director, Emergency Planning W. Dennis, Assistant General Counsel

SUMMARY OF FINDINGS

IR 05000247/2007-004; 07/01/2007 - 09/30/2007; Indian Point Nuclear Generating Unit 2; Fire

Protection, Maintenance Risk Assessment and Emergent Work Control, and Surveillance Testing.

The report covered a three-month period of inspection by resident and region-based inspectors.

Three findings of very low significance were identified. These findings were determined to be non-cited violations. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process.

Findings for which the significance determination process (SDP) does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a non-cited violation (NCV) of License Condition 2.K., fire protection program, because Entergy failed to identify a degraded three-hour rated fire door on the east entrance of the 12 fire main booster pump room. The door was determined to be inoperable due to a misalignment, which prevented the door from fully closing. Entergy entered this issue into their corrective action program, took immediate compensatory actions, realigned the door, and ensured that it would fully close.

The inspectors determined that this finding was more than minor because it was associated with the protection against external factors attribute of the Mitigating Systems cornerstone; and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding was evaluated using Phase 1 of Inspection Manual Chapter (IMC) 0609 Appendix F, Fire Protection Significance Determination Process. The inspectors determined that this issue was of very low safety significance because the degradation of the fire barrier was moderate based on the fire door displaying significant degradation affecting its performance or reliability.

However, it was still expected to provide some defense-in-depth benefit. Specifically, the fire door was expected to provide a minimum of 20 minutes fire endurance protection, and the in-situ fire ignition sources and flammable materials were positioned such that the degraded fire door would not be subject to direct flame impingement.

The inspectors determined that the finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy personnel who routinely traverse through or past the fire door had not identified the degraded condition. (P.1(a))

(Section 1R05)

Green.

The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, because Entergy did not ensure iv that procedures associated with operation of the safety injection (SI) system during venting were appropriate to the circumstances. Specifically, procedure 2-PT-M108,

RHR/SI [residual heat removal/safety injection] System Venting, did not have appropriate controls to ensure the safety injection piping and pumps remained operable during accident conditions. Entergy entered the issue into their corrective action program and revised the venting procedure to ensure operator actions are appropriately evaluated and credited to maintain operability of the system.

The inspectors determined that this finding was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone; and it impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. This finding was evaluated using Phase 1 of IMC 0609,

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609,</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Determining the Significance of Reactor Inspection Findings for At-Power Situations. The inspectors determined this finding resulted in a loss of function of a single train of SI for approximately five minutes. Because the total inoperability time was less than the allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, and the finding is not potentially risk significant due to a seismic, flooding, or severe weather initiating event, this finding screens as very low safety significance (Green).

The inspectors determined that this finding had a cross-cutting aspect in the area of human performance because Entergy did not ensure that complete, accurate and up-to-date procedures were available. (H.2(c)) (Section 1R22)

Cornerstone: Barrier Integrity

Green.

The inspectors identified a non-cited violation of 10 CFR 50 Appendix B,

Criterion XVI, Corrective Actions, in that, Entergy did not implement timely corrective actions for a degraded condition associated with the 25 Containment Fan Cooler Unit (FCU) flow indicator. Specifically, the failure to take timely corrective actions for the degraded service water flow indicator for the 25 FCU, initially identified in October 2006, resulted in the inability to ensure that sufficient service water flow was available for the component to perform its intended function. Subsequently, it was identified that a reduced service water flow condition did exist. Entergy entered the issue into their corrective action program and implemented corrective actions to restore adequate indication of service water flow to the 25 FCU. Entergy is evaluating maintenance practices to determine the appropriateness of a periodic blow-down of the transmitter impulse lines to prevent sediment buildup.

The inspectors determined that this finding was more than minor because it was associated with the structure, system, and component and barrier performance attribute of the Barrier Integrity cornerstone; and it impacted the cornerstone objective of providing reasonable assurance that the physical design barrier (containment) protects the public from radionuclide releases caused by accidents or events. This finding was evaluated using IMC 0609, Appendix H, Containment Integrity Significance Determination Process. This was determined to be a Type B finding because it potentially impacted containment integrity but did not result in the increased likelihood of an initiating event. This finding was determined to be of very low safety significance v because, while it could impact late containment failure, it did not impact a function that was important to large early release frequency.

The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy did not thoroughly evaluate the condition when initially identified. (P.1(c)) (Section 1R13)

B.

Licensee-Identified Violation

None.

REPORT DETAILS

Summary of Plant Status

Indian Point Nuclear Generating Unit 2 began the inspection period operating at full power and remained at or near full power throughout the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors reviewed the readiness of risk-significant systems for extreme weather conditions, and evaluated implementation of extreme hot weather procedures and compensatory measures during the period August 3, 2007 through August 12, 2007.

The inspectors conducted walkdowns of plant equipment, interviewed personnel, and reviewed operating procedures to ensure that two risk-significant systems during this condition (auxiliary feedwater and emergency diesel generators) would not be adversely affected by the hot weather. In addition, the inspectors reviewed offsite power reliability and protocols with the transmission operator to ensure the plant appropriately evaluated risk during these periods of hot weather. The documents reviewed are listed in the

. This review represented one inspection sample of risk significant systems.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

The inspectors performed partial system walkdowns to verify the operability of redundant or diverse trains and components during periods of system train unavailability or following periods of maintenance. The inspectors referenced the system procedures, the Updated Final Safety Analysis Report (UFSAR), and system drawings to verify that the alignment of the available train supported its required safety functions. The inspectors also reviewed applicable condition reports and work orders to ensure that Entergy had identified and properly addressed equipment discrepancies that could potentially impair the capability of the available train, as required by Title 10 of the Code of Federal Regulations (CFR) Part 50, Appendix B, Criterion XVI, Corrective Action.

The documents reviewed during these inspections are listed in the Attachment.

The inspectors performed partial walkdowns on the following systems which represented three inspection samples:

  • Fire protection system following 11 fire main booster pump testing.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Quarterly Inspection

a. Inspection Scope

The inspectors conducted a tour of several fire areas to assess the material condition and operational status of fire protection features. The inspectors verified, consistent with applicable administrative procedures, that: combustibles and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with Entergys fire protection program. The inspectors evaluated the fire protection program against the requirements of Licensee Condition 2.K. The documents reviewed are listed in the Attachment. This inspection represented 10 inspection samples for fire protection tours and were conducted in the following areas:

  • Fire Zone 23;
  • Fire Zone 10;
  • Fire Zone 4;
  • Fire Zone 12, 13, 24, and 25;
  • Fire Zone 14;
  • Fire Zone 14A, 15A, 16A, 17A, and 19A;
  • Fire Zone 361 and 362;
  • Fire Zone 74A and 74B;
  • Fire Zone 152; and
  • Fire Zone 3 and 29A.

b. Findings

Introduction:

The inspectors identified a Green non-cited violation (NCV) of License Condition 2.K., fire protection program, because Entergy failed to identify a degraded three-hour rated fire door on the east entrance of the 12 fire main booster pump room.

Description:

On September 6, 2007, the inspectors performed a fire protection walkdown of the 11 and 12 fire main booster pump areas. The inspectors noted that the three-hour rated, swing-type fire door on the east side of the 12 fire main booster pump cell would not close properly and left a gap along the perimeter of the door. The inspectors reviewed Entergys Fire Hazards Analysis Report and determined that the door is required to meet licensing commitments, and is designed to preclude the passage of flame and hot gases from the adjacent area. Degradation of this door could allow the propagation of a fire to impact the 12 fire main booster pump.

The inspectors informed shift operations personnel of the issue, and they determined the door was improperly aligned with the frame. Entergy evaluated the condition, took appropriate compensatory measures, realigned the door, ensured that it would fully close, and entered the condition into their corrective action program (CR-IP2-2007-03561). Additionally, the fire protection engineer was notified, and he determined that the door frame required replacement (CR-IP2-2007-03651).

The inspectors determined that this condition was a performance deficiency because the door was in a degraded condition that resulted in the fire barrier being non-functional. The inspectors determined it was reasonable that this condition should have been identified by Entergy because personnel routinely pass through the fire door, and the inability of the door to fully close was readily apparent. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRCs regulatory function, and the finding was not the result of any willful violation of NRC requirements.

Analysis:

The inspectors determined that this finding was more than minor because it was associated with the protection against external factors attribute of the Mitigating Systems cornerstone; and it affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors performed a Phase 1 screening of the deficiency in accordance with Inspection Manual Chapter (IMC) 0609 and evaluated the safety-significance using IMC 0609 Appendix F, Fire Protection Significance Determination Process. The issue was determined to be of very low safety significance because the degradation of the fire barrier was moderate based on the fire door displaying significant degradation affecting its performance or reliability. However, it was still expected to provide some defense-in-depth benefit. Specifically, the fire door was expected to provide a minimum of 20 minutes fire endurance protection, and the in-situ fire ignition sources and flammable materials were positioned such that the degraded fire door would not be subject to direct flame impingement.

The inspectors determined that the finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy personnel who routinely traverse through or past the fire door had not identified the degraded condition. (P.1(a))

Enforcement:

License Condition 2.K., fire protection program, requires that Entergy implement and maintain in effect all provisions of the NRC-approved fire protection program, as approved in part by the NRC Safety Evaluation Report (SER) dated January 31, 1979. The January 31, 1979, SER requires administrative controls comparable to those described in NRC Branch Technical Position 9.5-1, Guidelines for Fire Protection for Nuclear Power Plants Docketed Prior to July 1, 1976. Branch Technical Position (BTP) 9.5-1 requires that measures be established to assure that conditions adverse to fire protection, such as deficiencies, deviations, defective components, and non-conformities are promptly identified, reported, and corrected.

Contrary to the above, Entergy failed to promptly identify the degraded condition of the 12 fire main booster pump area fire door. Once identified by the inspectors, Entergy initiated CRs IP2-2007-03561 and IP2-2007-03651 documenting the deficiency in their corrective action program (CAP). Because the violation was of very low safety significance and entered into their CAP, this violation is being treated as an NCV per Section VI.A of the NRC Enforcement Policy: NCV 05000247/2007004-01, Degraded 12 Fire Main Booster Pump Cell Fire Door.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors reviewed Indian Point Nuclear Generating Unit 2s Individual Plant Examination and the UFSAR concerning internal flooding events. The inspection included a walkdown of accessible areas of the plant, including the service water pipe chase area of the primary auxiliary building. Inspectors evaluated these areas for potential susceptibilities to internal flooding and verified the assumptions included in the sites internal flooding analysis. The inspectors also reviewed relevant abnormal operating and emergency plan procedures. The documents reviewed are listed in the

. This inspection represented one sample for internal flood protection measures.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

On August 20, 2007, the inspectors observed licensed operator simulator training to verify that operator performance was adequate and that evaluators were identifying and documenting crew performance problems. The inspectors evaluated the performance of risk-significant operator actions, including the use of emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, the implementation of appropriate actions in response to alarms, the performance of timely control board operation and manipulation, and the oversight and direction provided by the shift manager. The inspectors also reviewed simulator fidelity with respect to the actual plant. Licensed operator training was evaluated against the requirements of 10 CFR Part 55, Operators Licenses. The documents reviewed during this inspection are listed in the Attachment. This observation of operator simulator training represented one inspection sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed performance-based problems that involved the selected structures, systems, or components (SSCs) to assess the effectiveness of the maintenance program. Reviews focused on:

  • Proper Maintenance Rule scoping in accordance with 10 CFR 50.65;
  • Characterization of reliability issues;
  • Changing system and component unavailability;
  • Identifying and addressing common cause failures;
  • Trending of system flow and temperature values;
  • Appropriateness of performance criteria for SSCs classified (a)(2); and
  • Adequacy of goals and corrective actions for SSCs classified (a)(1).

The inspectors also reviewed system health reports, maintenance backlogs, and Maintenance Rule basis documents. The inspectors evaluated the maintenance program against the requirements of 10 CFR Part 50.65. The documents reviewed during this inspection are listed in the Attachment. The following maintenance effectiveness samples were reviewed and represented three inspection samples:

  • Direct Current (DC) power; and
  • Appendix R lighting.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed maintenance activities to verify that the appropriate risk assessments were performed prior to removing equipment for work. The inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The documents reviewed during this inspection are listed in the Attachment.

The following activities represented five inspection samples:

  • Decreased indicated service water flow to 25 containment fan cooler unit;
  • 345 KiloVolt (KV) feeder W93 removed from service; and
  • Rod control circuit QC-412B replacement.

b. Findings

Introduction:

The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, in that, Entergy did not implement timely corrective actions for a degraded condition associated with the 25 containment fan cooler unit (FCU) service water flow indication.

Discussion: On September 16, 2007, Entergy conducted a quarterly surveillance to verify adequate cooling water flow through the containment FCUs. Entergy identified that the 25 FCU did not meet the minimum required flow, and declared the FCU inoperable. Entergy initiated corrective actions to restore flow to greater than the minimum required by Technical Specifications, and the 25 FCU was restored to an operable status on September 20, 2007.

The inspectors evaluated Entergys actions to restore adequate flow to the 25 FCU and reviewed the associated risk management actions during the emergent work. In addition, the inspectors reviewed the past work history associated with service water flow to the FCU. The inspectors identified that a condition report, CR-IP2-2006-05951, had been written on October 8, 2006, due to anomalous service water flow indications on 25 FCU during a valve stroke surveillance test. This issue was evaluated in the corrective action process, and it was determined that the most likely cause for the oscillating indication was excessive silting of the instrument lines to the flow transmitter.

A work order was written to blowdown the instrument lines associated with the transmitter, and the condition report was closed to the work order. The work order was coded as elective maintenance because Entergy determined that the deficiency was only associated with the flow indication, and did not represent an actual reduction in flow. This work order was not implemented. Entergy failed to consider that the valve alignment for the test in which the anomaly was identified was the same alignment as required by the quarterly surveillance to verify adequate service water flow to the containment fan cooler units. Condition report, CR-IP2-2007-03424, was written on August 28, 2007, that identified the same anomalous flow condition and a corrective action to blowdown the impulse lines was completed on August 30, 2007.

The inspectors reviewed the data obtained during the quarterly surveillance test for periods before, and after the anomalous flow condition was identified in October 2006.

Prior to the anomaly being identified, the flow for 25 FCU was routinely found to be in the range of 1760-1800 gallons per minute (gpm). After October 2006, the flow was recorded as being greater than 2000 gpm, with the exception of one instance where the flow was 1780 gpm. 2000 gpm is the maximum value in the indicating range of the meter. The inspectors determined that, based on the identified anomaly in the flow indication and the prompt change in indicated flow during the quarterly surveillance, the meter did not provide a reliable indication of actual system flow. Entergy determined that the actual reduction in service water flow through the 25 FCU identified on September 16, 2007, was the result of flow blockage in the system and most likely occurred during heavy rains, and a subsequent increase in river water silt and debris, during April 2007. The inspectors determined that the unreliable service water flow indication prevented earlier indication of the flow reduction through the quarterly surveillance test. Entergy implemented corrective actions to restore adequate service water flow indication to 25 FCU and is evaluating maintenance practices to determine the appropriateness of a periodic blowdown of the transmitter impulse lines to prevent sediment buildup.

The inspectors determined that the failure to take timely corrective action for a degraded condition was a performance deficiency and did not meet the requirements of 10 CFR 50 Appendix B, Criterion XVI, Corrective Actions. The cause of this performance deficiency was within Entergys ability to foresee and prevent, because Entergy did not fully evaluate anomalous flow indications on the 25 FCU in October 2006 and subsequent changes in flow rate during quarterly surveillance testing. Traditional enforcement does not apply since there were no actual safety consequences or potential for impacting the NRCs regulatory function, and the finding was not the result of any willful violation of NRC requirements or Entergys procedures.

Analysis:

The inspectors determined that this finding was more than minor because it was associated with the SSC and barrier performance attribute of the Barrier Integrity cornerstone; and it impacted the cornerstone objective of providing reasonable assurance that the physical design barrier (containment) protects the public from radionuclide releases caused by accidents or events. Specifically, the failure to take timely corrective actions for the degraded service water flow indicator for the 25 FCU, initially identified in October 2006, resulted in the inability to ensure that sufficient service water flow was available for the FCU to perform its intended safety function.

Subsequently, it was identified that a reduced service water flow condition did exist. The inspectors evaluated this finding using IMC 0609, Appendix H, Containment Integrity Significance Determination Process. This was determined to be a Type B finding because it potentially impacted containment integrity but did not result in the increased likelihood of an initiating event. This finding was determined to be of very low safety significance because, while it could impact late containment failure, it did not impact a function that was important to large early release frequency.

The inspectors determined that this finding had a cross-cutting aspect in the area of problem identification and resolution because Entergy did not thoroughly evaluate the condition when initially identified. Specifically, the evaluation did not address the impact of the degraded condition on the flow indication obtained during the quarterly surveillance, which ensures adequate service water flow. Therefore, the work order to blow-down the instrument lines was not appropriately prioritized to ensure the corrective action was performed in a timely manner. (P.1(c))

Enforcement:

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected. Contrary to the above, Entergy failed to correct a condition adverse to quality in a prompt manner, commensurate with its safety significance. Specifically, the corrective actions associated with the degraded service water flow indication, initially identified in October 2006, were not performed in a timely manner and resulted in the inability to promptly identify an actual degradation of service water flow to 25 FCU. Because of the very low safety significance of this finding and because the finding was entered into Entergys corrective action program as CR-IP2-2007-03706, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000247/2007004-02, Untimely Corrective Actions to Repair a Degraded Service Water Flow Instrument.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications. The inspectors' reviews included verification that the operability determinations were performed in accordance with procedure ENN-OP-104, "Operability Determinations." The inspectors assessed the technical adequacy of the evaluations to ensure consistency with the Technical Specifications, UFSAR, and associated design basis documents. The documents reviewed during this inspection are listed in the Attachment. The following operability evaluations were reviewed and represented five inspection samples:

  • CR IP2-07-03161, 23 Station battery charger found below TS surveillance criteria;

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and engineering personnel. The inspectors verified: test acceptance criteria were clear, tests demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Upon completion, the inspectors verified that equipment was returned to the proper alignment necessary to perform its safety function.

Post-maintenance testing was evaluated against the requirements of 10 CFR Part 50, Appendix B, Criterion XI, Test Control. The documents reviewed during this inspection are listed in the Attachment. The following post-maintenance activities were reviewed and represented six inspection samples:

  • WO IP2-06-26506, 23 coolant charging pump following mechanical seal replacement;

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems and components to assess whether they satisfied Technical Specifications, UFSAR, Technical Requirements Manual, and Entergy procedure requirements. The inspectors verified that: test acceptance criteria were clear, demonstrated operational readiness, and were consistent with design basis documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Following the test, the inspectors verified that the equipment was capable of performing the required safety functions. The inspectors evaluated the surveillance tests against the requirements in Technical Specifications. The documents reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented five inspection samples:

  • 2-PT-Q16, Containment fan cooler unit cooling water test;
  • 2-PT-M7, Analog rod position functional test;

b. Findings

Introduction:

The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, because Entergy did not ensure that procedures associated with operation of the safety injection (SI) system during venting were appropriate to the circumstances.

Description:

During observation of a monthly operations procedure to perform safety injection system venting in accordance with procedure 2-PT-M108, RHR/SI [residual heat removal/safety injection] System Venting, the inspectors noted the licensee did not declare the pumps or various safety injection subsystems inoperable during the actual venting process. In the case of the SI pump, which is vented every month, the procedure assumes the pump is operable. The inspectors questioned whether the pump remained operable with the casing vent open because some flow would not be available for core injection, and on sump recirculation the emergency core cooling system (ECCS) leakage outside the containment could be high. Entergy determined that the pump would not fulfill its safety function if the valve was left in the full open position. The inspectors reviewed the procedures to determine if credit would be reasonable for the operator to perform this manual action to close the valve instead of the function of the SI system to respond automatically. There were no procedure requirements in place to ensure that a dedicated operator would be present, in constant communication, and with appropriate guidance to take actions as needed if an event was to occur during the venting evolution. The inspectors concluded the pump should not be considered operable, because crediting manual operator action in lieu of the pump running automatically requires consideration of the manual actions needed to restore operability and reviewing them pursuant to 10 CFR 50.59. In addition, other possible piping vent paths are used in the procedure. Although these vents would only be used if gas voids are found in certain locations, there is a potential the vent could be used as the procedure directs. The procedure guidance for these paths was also deficient; crediting the operator to perform an action to ensure the SI system retained its safety function. The licensee wrote CR-IP2-2007-03032 to address these concerns.

The licensee revised procedures, providing detailed guidance crediting operator action, or in the case for some piping vents, changed the procedure to ensure the valve was not opened such that excess SI flow would be lost during venting.

The inspectors concluded that the procedure lacked adequate guidance to ensure the SI system remained operable by controlling valve positions or having detailed instructions to credit an operator to perform these actions. Entergy implemented corrective actions and revised the venting procedure to ensure operator actions were appropriately evaluated and credited to maintain operability of the system.

The inspectors determined that the failure to ensure that procedures associated with the venting of the SI lines were appropriate to the circumstances and included appropriate controls of plant equipment or dedicated operator was a performance deficiency and did not meet the requirements of 10 CFR 50 Appendix B, Criterion V, Instructions, Procedures, and Drawing. The cause of this performance deficiency was within Entergys ability to foresee and prevent, based on readily available NRC and industry guidance on maintaining the operability of systems during certain evolutions, such as venting. Traditional enforcement does not apply because there were no actual safety consequences or potential for impacting the NRCs regulatory function, and the finding was not the result of any willful violation of NRC requirements or Entergys procedures.

Analysis:

The inspectors determined that this finding was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone; and it impacted the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, procedure 2-PT-M108, RHR/SI System Venting, did not have appropriate controls to ensure the SI piping and pumps remained operable during accident conditions. This finding was evaluated using Phase 1 of IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations. The inspectors determined this finding resulted in a loss of function of a single train of SI for approximately five minutes. Because the total inoperability time was less than the allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, and the finding is not potentially risk significant due to a seismic, flooding, or severe weather initiating event, this finding screens as very low safety significance (Green).

The inspectors determined that this finding had a cross-cutting aspect in the area of human performance because Entergy did not ensure that complete, accurate and up-to-date procedures were available. Specifically, Entergy did not ensure that the venting procedure for the SI system had adequate guidance to ensure the SI system remained operable by controlling valve positions, or having detailed instructions to credit an operator to perform these actions. (H.2(c))

Enforcement:

10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, requires, in part, that activities affecting quality be prescribed by documented instructions or procedures of a type appropriate to the circumstances and include appropriate quantitative or qualitative acceptance criteria to determine that the activities were satisfactorily accomplished. Contrary to this, Entergys procedure for venting SI pumps and piping contained in 2-PT-M108, RHR/SI System Venting, did not contain instructions appropriate to the circumstances which would have ensured that the action was satisfactorily accomplished. Specifically, the procedure did not provide appropriate controls to ensure the SI piping and pumps remained operable during accident conditions. Because of the very low safety significance of this finding and because the finding was entered into Entergys corrective action program as CR-IP2-2007-03032, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000247/2007004-03, Procedure Inadequate to Ensure Operability of SI Pumps During Venting.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Evaluation (71114.02 - 1 Sample)

a. Inspection Scope

A region-based specialist inspector reviewed Entergys activities related to the existing Indian Point alert and notification system (ANS), and reviewed the progress made in the design and installation of a new siren system. This inspection was conducted in accordance with the baseline inspection program deviation authorized by the NRC Executive Director of Operations (EDO) in a memorandum dated October 31, 2005, and renewed by the EDO in a memorandum dated December 11, 2006.

The new siren system is being installed around the Indian Point Energy Center to satisfy commitments documented in an NRC Confirmatory Order (dated January 31, 2006) that implements the requirements outlined in the 2005 Energy Policy Act. In January 2007, Entergy requested an extension of the deadline for completing the ANS project as described in the Confirmatory Order. The Confirmatory Order set a January 30, 2007, deadline for completing installation. Entergys extension request cited several issues that were beyond their control, as the basis for the delay. On January 23, 2007, the NRC granted Entergys extension request and established April 15, 2007, as the new installation completion date. The licensee conducted a full-system demonstration test of the new ANS on April 12, and the results of that test failed to meet the acceptance criteria for the new system. On April 13, 2007, Entergy requested another extension which was subsequently denied. On April 23, 2007, the NRC issued a Notice of Violation (NOV) and civil penalty for Entergys failure to comply with the siren operability date in the Confirmatory Order. On May 23, 2007, Entergy responded to the NOV and committed to August 24, 2007, as the latest date anticipated for declaring the new ANS operable.

On August 30, the NRC issued a NOV to Entergy due to its failure to take timely and necessary actions to ensure the Federal Emergency Management Agencys (FEMA)approval for the use of the ANS by August 24, 2007. On September 12, 2007, FEMA issued a letter indicating that the new ANS was not adequate in the areas of acoustics, sound blockage from foliage, and control systems. In a letter dated September 21 2007, Entergy requested a meeting with FEMA to discuss the technical aspects of Entergys proposed plans and determine a mutually acceptable schedule for resolving the open items.

The inspectors conducted the following onsite inspection activities during this quarter:

  • Observed the full-volume sounding to obtain far-field acoustical data (August 9, 2007); and
  • Met with Entergy representatives to discuss and obtain complete back-up battery testing results (August 13 - 14, 2007).

The inspectors also inspected the status of and corrective actions for the current ANS to assure that Entergy was appropriately maintaining the system, including the quarterly full-system growl test of the current ANS to demonstrate its functionality. Inspectors were on site on September 12, 2007, to observe and verify the performance of the current ANS during the annually-conducted full-volume test of the current ANS.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

2OS1 Access Control to Radiologically Significant Areas (71121.01 - 14 samples)

a. Inspection Scope

During July 16 through 19, 2007, the inspectors conducted the following activities to verify that the licensee was properly implementing physical, engineering, and administrative controls for access to high radiation areas, and other radiologically controlled areas, and that workers were adhering to these controls when working in these areas. Implementation of the access control program was reviewed against the criteria contained in 10 CFR 20, Technical Specifications, and the licensees procedures.

(1) There were no occupational exposure cornerstone performance indicator incidents during the current assessment period.
(2) The inspectors walked down exposure significant work areas of the plant (both Units 2 and 3) and reviewed licensee controls and surveys to determine if licensee surveys, postings, and barricades were acceptable and in accordance with regulatory requirements.
(3) The inspectors walked down exposure significant work areas of the plant (both Units 2 and 3) and conducted independent surveys to determine whether prescribed radiation work permit and procedural controls were in place and whether licensee surveys and postings were complete and accurate.
(4) There were no internal dose assessments greater than 50 mrem during 2007.
(5) The licensees physical and programmatic controls for highly activated materials stored underwater in the Unit 2 and Unit 3 spent fuel pools were reviewed and evaluated through observation and a review of the applicable access control procedure.
(6) A review of licensee radiation protection program self-assessments and audits during 2007 was conducted to determine if identified problems were entered into the corrective action program for resolution.
(7) Seven condition reports associated with the radiation protection access control and ALARA areas between March 2007 and July 2007, were reviewed and discussed with licensee staff to determine if the follow-up activities were being conducted in an effective and timely manner commensurate with their safety significance.
(8) Based on the condition reports reviewed, repetitive deficiencies were screened to determine if the licensees self-assessment activities were identifying and addressing these deficiencies.
(9) There were no Occupational Exposure Performance Indicator incidents reported during the current assessment period.
(10) Changes to the high radiation area and very high radiation area procedures since the last inspection in this area were reviewed and management of these changes were discussed with the Radiation Protection Manager.
(11) Controls associated with potential changing plant conditions to anticipate timely posting and controls of radiation hazards was discussed with a radiation protection supervisor.
(12) All accessible locked high radiation area entrances in both Units 2 and 3 were verified to be locked through challenging the locks or doors.
(13) Several radiological condition reports were reviewed to evaluate if the incidents were caused by radiation worker errors and determine if there were any trends or patterns and if the licensees corrective actions were adequately addressing these trends.
(14) Several radiological condition reports were reviewed to evaluate if the incidents were caused by radiation protection technician errors and determine if there were any trends or patterns and if the licensees corrective actions were adequately addressing these trends.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02 - 2 samples)

a. Inspection Scope

During July 16 through 19, 2007, the inspectors conducted the following activities to verify that the licensee was properly maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). Implementation of the ALARA program was reviewed against the criteria contained in 10 CFR 20.1101(b) and the licensees procedures.

(1) The procedure and methodology for adjusting work activity exposure estimates was evaluated to include revisions for emergent work and unexpected radiological conditions. The methodology for the exposure estimate adjustments was evaluated with respect to sound radiation protection and ALARA principles and to ensure the revised exposure estimates provided an effective ALARA performance measure.
(2) Based on the condition reports reviewed, repetitive deficiencies in the ALARA program were screened to determine if the licensees self-assessment activities were identifying and addressing these deficiencies.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

[OA]

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed performance indicator (PI) data for the cornerstones listed below and used Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, to verify individual PI accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment.

Mitigating Systems Cornerstone

Barrier Integrity Cornerstone

The inspectors reviewed data and plant records from the above noted periods. The records included PI data summary reports, licensee event reports, operator narrative logs, the licensee corrective action program, and Maintenance Rule records. The inspectors verified the accuracy of the number of critical hours reported, and interviewed the system engineers and operators responsible for data collection and evaluation.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Problem Identification and Resolution (PI&R) Program Review

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergys corrective action program. The review was accomplished by accessing Entergys computerized database for condition reports (CRs) and attending CR screening meetings.

In accordance with the baseline inspection modules, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for additional follow-up and review. The inspectors assessed Entergys threshold for problem identification, the adequacy of the cause analyses, extent of condition reviews, operability determinations, and the timeliness of the specified corrective actions. The CRs reviewed during this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

4OA3 Event Followup

.1 Operations performance during single control rod drop of 20 steps on August 23, 2007

a. Inspection Scope

The inspectors observed control room personnel response during an unexpected control rod drop on August 23, 2007, that occurred during control rod surveillance testing. During control rod exercise testing of Shutdown Bank B, control rod G-3 dropped from 213 steps to 198 steps with no operator action. The inspectors observed Entergys response in the control room to verify that plant equipment response was appropriately evaluated, and to ensure that operating procedures were being appropriately implemented. The inspectors discussed the event and corrective actions with plant management in order to confirm that Entergy had taken appropriate corrective actions in restoring the plant. The documents reviewed are included in the Attachment.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 Groundwater Contamination Investigation

a. Inspection Scope

Continued inspection of Entergys plans, procedures, and characterization activities affecting the contaminated groundwater condition at Indian Point, relative to NRC regulatory requirements, was authorized by the NRC Executive Director of Operations in a Reactor Oversight Process deviation memorandum dated October 31, 2005 (ADAMS Accession Number ML053010404) and renewed on December 11, 2006 (ADAMS Accession Number ML063480016). Accordingly, continuing oversight of licensee progress has been conducted throughout this quarterly inspection report period, which included: onsite review of licensee performance, progress, and achievements; independent split sample analyses of selected monitoring wells; expanded sampling of the edible portions of various fish collected from multiple locations in the Hudson River; review of an onsite underground auxiliary steam pipe leak; and frequent communication of NRC observations with interested Federal, State, and local government stakeholders.

In July and August 2007, NRC staff and U.S. Geological Survey (USGS) scientists, in consultation with representatives of New York State Department of Environmental Conservation, conducted an independent assessment of selected data and information developed by Entergy and its geophysical contractor relative to fracture flow modeling, and groundwater characterization relative to flow and transport.

The methodology applied by USGS utilized data collected from downhole geophysical and flow logs conducted by Geophysical Applications, Inc, under the direction of the Entergys principal contractor for the groundwater investigations, GeoEnvironmental, Inc. (GZA).

The geophysical data (i.e., caliper, optical and acoustic televiewer, fluid resistivity and temperature logs), fracture mapping and flow logs were processed and visualized with a computer-based system, WELLCAD. The method permitted a systematic mapping of fracture orientations, density, associated flow conditions and properties using composite portrayals of vertical plots of the geophysical logs and hydraulic test data and analyses.

These composite portrayals facilitated comparisons and analyses of selected IPEC monitoring wells for the determination of the location and direction of discrete high flow zones, including associated flux and transmissivity. It is expected that the information and analyses will aid the NRC and USGS staff in evaluations of GZAs conceptual groundwater flow and transport model that was derived from previous hydraulic pump and tracer tests conducted on selected monitoring wells.

b. Findings and Observations

No findings of significance were identified.

The fracture flow assessment provided an effective means of visualizing fracture zones and properties of certain IPEC monitoring wells; and provided an enhanced conceptualization of groundwater flow and transport characteristics which is important to the NRCs overall assessment of the licensees groundwater modeling and characterization. The NRC and USGS will apply the knowledge gained from this assessment for independent review of Entergys characterization of groundwater behavior, its selection of monitoring locations and performance indicators for long-term site groundwater monitoring, and its determination of remediation strategies, as appropriate. This assessment provides another tool to be used to effectively verify and validate that Entergys groundwater modeling and dose assessment methods continue to assure that public health and safety, and protection of the environment is maintained.

During this period, the NRC continued split sampling of selected monitoring wells for independent analysis by the Oak Ridge Institute for Science and Education, Environmental Site Survey and Assessment Program (ORISE/ESSAP) radioanalytical laboratory. The NRCs assessment of the licensees sample analytical results data indicated that the licensees analytical contractor reported final sample results that were comparable with the NRCs analytical results.

Fish samples were also split and independently analyzed during this period. The samples were collected from three separate locations on the Hudson River (i.e., an area in the near vicinity of the plant, the Roseton control location (20-30 miles, up river), and the Catskills region (about 80 to 90 miles, up river)). The NRC analyzed edible portions of the fish samples, commensurate with the requirements of the environmental monitoring program and the existing pathway for exposure from liquid radiological releases to the Hudson River. None of the 18 samples indicated any detectable radioactivity distinguishable from background (i.e., all samples were less than the Minimum Detectable Activity established by ORISE for gamma and strontium-90 radionuclides).

The NRCs ORISE/ESSAP sample results are available in ADAMS under the following Accession Numbers: ML072840255, ML072840278, ML072840292, ML072840312, ML072840323, ML072840334, ML072840357. To date, plant-related radioactivity has not been detected in any of the sites southern boundary wells or offsite environmental groundwater monitoring locations. Information collected and assessed to-date, continues to support that the estimated radiological release fraction through groundwater is negligible relative to NRC regulatory limits.

On April 7, 2007, two separate underground steam leaks were detected emanating through the asphalt surfaces west and north of Unit 3. The affected 8" auxiliary steam line was isolated on April 23, 2007, and subsequently excavated and replaced. As expected, a very low tritium concentration was detected in the area, likely due to normal tritium diffusion or deposition onsite, Condition Report No. CR-IP3-2007-1852 pertains. Entergy performed a very conservative bounding evaluation of the resulting ground and air releases that indicated approximately 1E-8 mrem/yr and 2E-6 mrem/yr due to the liquid and air release pathways, respectively. Such releases are not considered significant and are below reporting requirements.

4OA6 Meetings, including Exit

Exit Meeting Summary

On October 3, 2007, the inspectors presented the inspection results to Mr. Anthony Vitale and other Entergy staff members, who acknowledged the inspection results presented.

Entergy did not identify any material as proprietary.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Entergy Personnel

B. Christman, Manager of Training and Development
P. Conroy, Director of Nuclear Safety Assurance
F. Dacimo, Site Vice President
R. Hansler, Reactor Engineering Superintendent
T. Jones, Licensing Supervisor
S. Manzione, Component Engineering Supervisor
B. McCarthy, Indian Point Unit 2 Assistant Operations Manager
E. ODonnell, Indian Point Unit 2 Operations Manager
T. Orlando, Director of Engineering
D. Parker, Maintenance Superintendent
B. Ray, Maintenance Superintendent
B. Sullivan, Emergency Planning Manager
P. Studley, Planning, Scheduling, and Outage Manager
M. Vasely, Balance of Plant System Engineering Supervisor
S. Verrochi, System Engineering Manager
A. Vitale, General Manager of Plant Operations
R. Walpole, Licensing Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000247/2007004-01

NCV

Degraded 12 Fire Main Booster Pump Cell Fire Door. (Section 1R05)

05000247/2007004-02

NCV

Untimely Corrective Actions to Repair a Degraded Service Water Flow Instrument.

(Section 1R13)

05000247/2007004-03

NCV

Procedure Inadequate to Ensure Operability of SI Pumps During Venting. (Section 1R22)

LIST OF DOCUMENTS REVIEWED