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| number = ML090300249
| number = ML090300249
| issue date = 01/29/2009
| issue date = 01/29/2009
| title = 01/22/09, Oconee Regulatory Conference, Unanticipated Reduction in Unit 1, RCS Inventory During Shutdown Conditions
| title = Regulatory Conference, Unanticipated Reduction in Unit 1, RCS Inventory During Shutdown Conditions
| author name =  
| author name =  
| author affiliation = Duke Energy Corp
| author affiliation = Duke Energy Corp
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{{#Wiki_filter:Oconee Nuclear StationRegulatory ConferenceUtiitdRdtiiUit1Enclosure 31 U nan ti c i pa t e d R e d uc ti on i n U n it 1 RCS Inventory During Shutdown ConditionsNRC Region II OfficeAtlanta, GeorgiaJanuary 22, 2009 Duke ParticipantsDave BaxterOconee Site Vice PresidentPreston GillespieOconee Station ManagerEddie AndersonOconee Operations SuperintendentRich Freudenber g e r Oconee Safet y Assurance Mana g e rEnclosure 32 g ygSteve NaderDuke PRA Engineering SupervisorBryan CarrollDuke PRA EngineerGraham DavenportOconee Regulatory Compliance ManagerDave CoyleOconee Operations Support ManagerBob MeixellOconee Regulatory Compliance EngineerJeff ThomasDuke Regulatory Compliance Manager AgendaOpening RemarksInitial Plant ConditionsEvent DiscussionPRA DiscussionRootCausesandCorrectiveActionsEnclosure 33Root Causes and Corrective Actions Closing Remarks Opening RemarksThe circumstances that led to the unplanned Loss of Inventory (LOI) did not meet Duke expectationsInadequate Automatic Voltage Regulator (AVR) maintenance procedure IP/0/B/2005/001 resulted in main generator lockout and slow transfer of powerEnclosure 34Failure to follow IP/0/A/3011/013A resulted in an ove r-current trip of the 1XP emergency feeder breaker due to an improperly set instantaneous magnetic trip deviceDuke agrees that the inadequate AVR maintenance procedure constituted a performance deficiency and a finding Opening RemarksTwo root cause analyses were performedLoss of backcharge source during AVR maintenance1XP 600 volt AC system failed to re-energize as expected Prompt, thorough and comprehensive actions implementedAnEventInvestigationTeamperformedanindependentEnclosure 35An Event Investigation Team performed an independent review of causal analyses and action plansThe LOI event has been factored into the Oconee Recovery Plan Opening RemarksDuring the event:Reactor Coolant System (RCS) level never decreased to the reduced inventory level (3 feet below flange)Event was quickly and correctly recognized and diagnosedOperators quickly entered the appropriate proceduresRCSlevelwasrestoredwithin17minutesEnclosure 36RCS level was restored within 17 minutesThere was no core damage, no offsite release, and containment integrity was not compromisedProcesses would not have prevented the event from occurring during periods of higher risk; however, additional controls would be in place to help recognize and mitigate the event  There are key differences between Duke's risk analysis and the risk analysis performed by the NRC Initial Plant Conditions Event DescriptionEnclosure 37Eddie Anderson, Oconee Operations Superintendent Initial Plant ConditionsDay 4 of Unit 1 EOC24 Refu eling Outage (April 15, 2008)Reactor in Cold Shutdown (Mode 6), RV head detensioned but still in place, and the equipment hatch was closedRCS ConditionsRCSlevel70inchesonLT
{{#Wiki_filter:Oconee Nuclear Station Regulatory Conference U
-5(84inchesisRVflange)Enclosure 38RCS level 70 inches on LT 5 (84 inches is RV flange)RCS temperature 96 FLow Pressure Injection (LPI) Trains A and B in serviceLPI in normal shutdown purification mode Initial Plant ConditionsAdditional sources of RCS makeup:Borated Water Storage Tank (BWST; 360,000 gallons)Bleed Holdup Tank (BHUT; 60,000 gallons)Bleed Transfer Pump 1A availableLPI Pump 1C availableEnclosure 39HPI Trains 1A and 1B availableElectrical power supplied by backcharged main transformerAlternate power from switchyard available through startup transformerAll emergency power sources availableFirst-time performance of Automatic Voltage Regulator (AVR) Maintenance Procedure IP/0/B/2005/001 Event DiscussionInterruption and restoration of control power to AVR actuated the K31 relay that caused Main Generator LockoutAs designed, a slow transfer of auxiliary power to startup transformer restored Decay Heat Removal (DHR) in ~ 2 secondsEnclosure 310MCC-1XP failed to re-energize as expectedCertain Air Operated Valves on the purification loop failed closed due to loss of solenoid power from 1XPPurification valves repositioning caused LPI Pump discharge pressure to lift purification relief valve Event DiscussionApproximate Timeline1323 -Unit 1 momentary interruption of power (~ 2 seconds)1324 -Operators immediately check LPI status, review activated Statalarms, silence alarms, determine RV level decreasing from computer trend1325 -AP/1/A/1700/026 (Loss of DHR) entered due to decreasing RCS level Enclosure 3111326 -Operators determine normal makeup lost and dispatch NEOs to open 1LP-21 (BWST Supply to LPI)  -Operator dispatched to close 1LP-96 (Purification Isolation)1338 -RCS level at ~ 54.5" on LT-5 (lowest level observed)-1LP-21 throttled open  1340 -RCS Level at ~ 72" on LT-5 (level restored) 1344 -1LP-21 closed. 1LP-96 closed to isolate purification to stop loss of RCS inventory. Approximately 2000 gallons of RCS transferred to MWHUT Event DiscussionLOI event was promptly recognized by multiple operators from computer trends and mitigated. Level was restored within 17 minutesOperator stress levels did not impact event mitigationDHR repowered automaticallyAlarms silenced within minutesEvent and mitigation not complicated (only system in service was DHR)Enclosure 312Additional mitigating equipment available per Defense In Depth (DID) sheets and use was proceduralizedLPI Injection from BWST (2 trains/2 pumps)HPI Injection from BWST (2 trains/2 pumps)BWST inventory at 360,000 gallons Extensive oversight to assist control room operatorsOperators had > 180 minutes to recognize and mitigate the LOI prior to core damage PRA DiscussionSteveNaderPRAEngineeringSupervisorEnclosure 313 Steve Nader , PRA Engineering Supervisor
ti i t d R d ti i
U it 1 1
Unanticipated Reduction in Unit 1 RCS Inventory During Shutdown Conditions NRC Region II Office Atlanta, Georgia January 22, 2009


PRA DiscussionThe CCDP for this event is approximately 3.8E-07The primary differences between Duke's risk analysis and the risk analysis performed by the NRC are 1.Treatment of 1XP failure 2.Timin g of the even tEnclosure 314 g 3.Credit for additional personnel 4.Dependency of human actions 5.Operator stress levelDependency Cut-off PRA Sensitivity ResultsWindow of Vulnerability PRA Discussion 1.Treatment of 1XP failureFailure of 1XP is an independent failure unrelated to the performance deficiency identified in the SDPInstead of setting the event to 1.0 or TRUE, it should be based on the probability of an incorrect breaker settingEnclosure 315Per Duke Root Cause, this was a random failure of the technician to properly set the breakerInspections demonstrated that similar breakers were set properlyInterview with responsible technician supports the conclusion that this was an independent, random failureDuke calculated failure rate is 3.0E-02Considering this credit alone, revised CCDP would be 4.7E-07 PRA Discussion 2.Timing of the eventRefer to drawing and timelineTime to midloop is significantly longer than assumed in the initial evaluations by Duke and NRCOperators have 100 minutes instead of the assumed 70 minutesEnclosure 316This should be classified as "expansive" time, changing the multiplier by a factor of 10 (0.1 to 0.01)Considering this credit alone, revised CCDP would be 4.9E-06 PRA DiscussionEnclosure 317 PRA DiscussionONS LOI Event TimelineEventMidloopLP 96 Closed -Event EndsLP 21 O pened -Makeu p StartsOperators Enter AP for LOIOperators Dispatched to Open LP 21 and Close LP 96Enclosure 318050100150200Time (minutes)Draindown via Purification Relief ValveHeatup and BoiloffCore Damage Occurs PRA Discussion 3.Credit for additional personnelShared Control Room -two complete crews and supporting shift personnel including OSM and STAIn excess of 15 people including management and author of EOP and APEnclosure 319SDP evaluation is dominated by failure to recognize the LOI, yet no credit is given for these additional expertsModest credit directly reduces the calculated significance of
Duke Participants Dave Baxter Oconee Site Vice President Preston Gillespie Oconee Station Manager Eddie Anderson Oconee Operations Superintendent Rich Freudenberger Oconee Safety Assurance Manager 2
g y
g Steve Nader Duke PRA Engineering Supervisor Bryan Carroll Duke PRA Engineer Graham Davenport Oconee Regulatory Compliance Manager Dave Coyle Oconee Operations Support Manager Bob Meixell Oconee Regulatory Compliance Engineer Jeff Thomas Duke Regulatory Compliance Manager


the eventConsidering this credit alone, revised CCDP would be low E-06 to mid E-06 PRA Discussion 4.Dependency of Human ActionsHuman errors and the evaluation of their interdependence drives the SDP conclusionSubjective determination (contrary to the SDP goal to be
Agenda Opening Remarks Initial Plant Conditions Event Discussion PRA Discussion Root Causes and Corrective Actions 3
Root Causes and Corrective Actions Closing Remarks


objective)Enclosure 320Dominant cutset contains two human errorsFailure to diagnose event (cognitive)Failure to inject when level reaches midloop (cognitive/execution)Dependency is more accurately evaluated by splitting the second action into its two parts (cognitive and execution)Considering this credit alone, revised CCDP would be 5.7E-06 PRA Discussion 5.Operator stress levelA key input to determining the failure to diagnose the eventPower interruption was less than 2 secondsDecreasing inventory was quickly and correctly recognizedMulti ple alarms silenced within minutesEnclosure 321 pAmple time available to diagnose and mitigate (100 minutes to midloop)Nominal stress is more appropriateConsidering this credit alone, revised CCDP would be approximately 1E-05 Dependency Cut-OffDependency Cut-off not used in actual SDP but can become importantSDP evaluation cites NUREG good practice which proposes a cap of 1E-05If applied, findings analyzed via the Shutdown SDP (which is Enclosure 322HRA driven) will be Yellow -not a useful insigh tPrevious Shutdown SDP findings have been characterized by the NRC as Green or WhiteDraft Low Power/Shutdown ANS Standard does not specify a limit -no industry consensus PRA Sensitivity ResultsFactorDiscussionRevised CCDP for each issue ColorTreatment of 1XPFailure of 1XP is a latent e rror independent of the performance deficiency4.7E-07GreenTiming of Event> 100 minutes available to Mid-Loop vs. 70 minutes4.9E-06WhiteEnclosure 323Additional PersonnelAdditional personnel i ndependent of the operating crew were availableLow E-06 toMid E-06WhiteDiagnosis and Action Depen denciesAction component of HEP is not dependent on cognitive component5.7E-06WhiteOperator StressStress levels normal versus high~1E-05White -Yellow Window of VulnerabilityEvent significance is very dependent on when it occurredMidloop operation --Reduced time to core damage; SDP result may be an order of magnitude higherRefueling canal flooded --Increased time to core damage; SDP result ma y be an order of ma g nitude lowe rEnclosure 324 ygUnit in No Mode --Event would not occurNot in backcharge alignment --Event would not occur PRA Overview/ConclusionsSDP for Shutdown Events is very dependent on human error evaluation and "stretches" the capabilities of HRA AnalysisReasonable analysts can reach quantitative conclusions that differ by an order of magnitudeQuantitative results should be balanced by qualitative factorsEnclosure 325Multiple independent cues throughout the even tAdditional sources of RCS makeupAll required equipment availableAdequate procedural guidance to mitigate the eventAmple time to respondAdditional personnel to respond to the eventDuke's calculated CCDP for this event is approximately 3.8E-07 Root Causes and Corrective ActionsPrestonGillespieOconeeStationManagerEnclosure 326 Preston Gillespie , Oconee Station Manager Root Causes and Corrective ActionsTwo separate root cause analyses were performedLoss of backcharge source during AVR maintenance1XP did not re-energize as expectedPrompt, thorough and comprehensive actions implemented AnindependentEventInvestigationTeamwasformedtoEnclosure 327An independent Event Investigation Team was formed toValidate/determine causes and contributing causesEnsure appropriate corrective and enhancement actions  The LOI event has been factored into the Oconee Recovery Plan Root Causes and Corrective ActionsRoot Cause (Loss of Backcharge Source)Failure to recognize an unanticipated system interaction between the AVR trip circuitry and the backcharge power path.
Opening Remarks The circumstances that led to the unplanned Loss of Inventory (LOI) did not meet Duke expectations 3/4 Inadequate Automatic Voltage Regulator (AVR) maintenance procedure IP/0/B/2005/001 resulted in main generator lockout and slow transfer of power 4
During the development and review of procedure IP/0/B/2005/001, preparers and reviewers did not recognize thatinterruptionandrestorationofcontrolpowertotheAVREnclosure 328 that interruption and restoration of control power to the AVR would actuate the K31 relay. Thus, steps to isolate actuation of the K31 relay were not includedContributing CauseBackcharging Procedure OP/1/A/1107/005 did not provide isolation from unnecessary trip signals Root Causes and Corrective ActionsActions Taken or Planned (Loss of Backcharge Source)Comprehensive action plan includes dozens of action items  AVR maintenance procedure IP/0/B/2005/001 placed on hold and later revised to appropriately address backcharge pathReviewed work activities planned during backcharging and Enclosure 329rescheduled many to when unit auxiliaries are on the startup transformer  Reviewed outage-related first-use procedures for risk impact OP/1,2,3/A/1107/005 revised to isolate unnecessary trips and ensure protected trains are adequate Root Causes and Corrective ActionsActions Taken or Planned (Loss of Backcharge Source)AP-26 revised to enhance existing mitigation strategiesUpgraded simulator to model RCS conditions during outage Performed LOI assessmentEstablished administrative controls similar to reduced inventory Enclosure 330controls prior to dropping RCS loopsBlocked open AOVs in LPI purification loopEliminated use of LPI purification when in reduced inventoryPlan to enhance Nuclear System Directives 403 and 703Formally establish electrical work integration team Root Causes and Corrective ActionsRoot Cause (1XP did not re-energize as expected)Failure to follow procedure. During the last breaker PM (1EOC23), the breaker technician failed to restore the breaker setting to the as-found HI instantaneous settingContributing CausesEnclosure 331Procedure did not have a place keeper nor did it require concurrent verification for the breaker settingAdditional outage loads increased inrush on the breaker above the LO trip setpoint (not an issue with breaker set to HI)
3/4 Failure to follow IP/0/A/3011/013A resulted in an over-current trip of the 1XP emergency feeder breaker due to an improperly set instantaneous magnetic trip device Duke agrees that the inadequate AVR maintenance procedure constituted a performance deficiency and a finding
Root Causes and Corrective ActionsActions Taken or Planned (1XP issue)Comprehensive action plan includes numerous actions  1XP-F3A breaker magnetic trip setting returned to HIIP/0/A/3011/013A revised to include concurrent verification for breaker setting (extent of condition review planned)Enclosure 332Reviewed loads off 1XP and scheduling of associated transfer of power procedures to minimize risk  Reviewed MCC breaker settings for 600 Volt molded case normal and emergency feeder breakers Plan to perform breaker coordination study Closing RemarksDaveBaxterOconeeSiteVicePresidentEnclosure 333 Dave Baxter , Oconee Site Vice President Closing RemarksWe understand and accept the findingThe circumstances that led to the unplanned LOI did not meet Duke expectationsOperators promptly recognized the LOI, quickly silenced alarms , and entered the a pp ro p riate p roceduresEnclosure 334,ppppThere was adequate mitigation capability Ample time was available to diagnose and mitigate the event Duke's calculated CCDP for the actual event is ~ 3.8E-07 Closing RemarksProcesses would not have prevented the event from occurring during periods of higher risk; however, additional controls would be in place to help recognize and mitigate the event  Two root cause analyses were performedProm p t , thorou gh and com prehensive actions im plemented Enclosure 335p,gppAn independent Event Investigation Team was formed to validate causes and contributing causes and ensure appropriate corrective and enhancement actions Closing RemarksDuke clearly recognizes the vital safety function performed by DHR during shutdown conditions and the importance of p ro per outa ge mana gement to reduce the likelihood and Enclosure 336ppggconsequences of shutdown events Simplified LPI Purification DiagramEnclosure 337}}
 
Opening Remarks Two root cause analyses were performed 3/4 Loss of backcharge source during AVR maintenance 3/4 1XP 600 volt AC system failed to re-energize as expected Prompt, thorough and comprehensive actions implemented An Event Investigation Team performed an independent 5
An Event Investigation Team performed an independent review of causal analyses and action plans The LOI event has been factored into the Oconee Recovery Plan
 
Opening Remarks During the event:
3/4 Reactor Coolant System (RCS) level never decreased to the reduced inventory level (3 feet below flange) 3/4 Event was quickly and correctly recognized and diagnosed 3/4 Operators quickly entered the appropriate procedures 3/4 RCS level was restored within 17 minutes 6
3/4 RCS level was restored within 17 minutes 3/4 There was no core damage, no offsite release, and containment integrity was not compromised Processes would not have prevented the event from occurring during periods of higher risk; however, additional controls would be in place to help recognize and mitigate the event There are key differences between Dukes risk analysis and the risk analysis performed by the NRC
 
Initial Plant Conditions Event Description 7
Eddie Anderson, Oconee Operations Superintendent
 
Initial Plant Conditions Day 4 of Unit 1 EOC24 Refueling Outage (April 15, 2008)
Reactor in Cold Shutdown (Mode 6), RV head detensioned but still in place, and the equipment hatch was closed RCS Conditions 3/4 RCS level 70 inches on LT-5 (84 inches is RV flange) 8 3/4 RCS level 70 inches on LT 5 (84 inches is RV flange) 3/4 RCS temperature 96 F 3/4 Low Pressure Injection (LPI) Trains A and B in service 3/4 LPI in normal shutdown purification mode
 
Initial Plant Conditions Additional sources of RCS makeup:
3/4 Borated Water Storage Tank (BWST; 360,000 gallons) 3/4 Bleed Holdup Tank (BHUT; 60,000 gallons)
Bleed Transfer Pump 1A available LPI Pump 1C available 9
HPI Trains 1A and 1B available Electrical power supplied by backcharged main transformer Alternate power from switchyard available through startup transformer All emergency power sources available First-time performance of Automatic Voltage Regulator (AVR) Maintenance Procedure IP/0/B/2005/001
 
Event Discussion Interruption and restoration of control power to AVR actuated the K31 relay that caused Main Generator Lockout As designed, a slow transfer of auxiliary power to startup transformer restored Decay Heat Removal (DHR) in ~ 2 seconds 10 MCC-1XP failed to re-energize as expected Certain Air Operated Valves on the purification loop failed closed due to loss of solenoid power from 1XP 3/4 Purification valves repositioning caused LPI Pump discharge pressure to lift purification relief valve
 
Event Discussion Approximate Timeline 1323 - Unit 1 momentary interruption of power (~ 2 seconds) 1324 - Operators immediately check LPI status, review activated Statalarms, silence alarms, determine RV level decreasing from computer trend 1325 - AP/1/A/1700/026 (Loss of DHR) entered due to decreasing RCS level 11 1326 - Operators determine normal makeup lost and dispatch NEOs to open 1LP-21 (BWST Supply to LPI)
- Operator dispatched to close 1LP-96 (Purification Isolation) 1338 - RCS level at ~ 54.5 on LT-5 (lowest level observed)
- 1LP-21 throttled open 1340 - RCS Level at ~ 72 on LT-5 (level restored) 1344 - 1LP-21 closed. 1LP-96 closed to isolate purification to stop loss of RCS inventory. Approximately 2000 gallons of RCS transferred to MWHUT
 
Event Discussion LOI event was promptly recognized by multiple operators from computer trends and mitigated. Level was restored within 17 minutes Operator stress levels did not impact event mitigation 3/4 DHR repowered automatically 3/4 Alarms silenced within minutes 3/4 Event and mitigation not complicated (only system in service was DHR) 12 Additional mitigating equipment available per Defense In Depth (DID) sheets and use was proceduralized 3/4 LPI Injection from BWST (2 trains/2 pumps) 3/4 HPI Injection from BWST (2 trains/2 pumps) 3/4 BWST inventory at 360,000 gallons Extensive oversight to assist control room operators Operators had > 180 minutes to recognize and mitigate the LOI prior to core damage
 
PRA Discussion Steve Nader PRA Engineering Supervisor 13 Steve Nader, PRA Engineering Supervisor
 
PRA Discussion The CCDP for this event is approximately 3.8E-07 The primary differences between Dukes risk analysis and the risk analysis performed by the NRC are 1.
Treatment of 1XP failure 2.
Timing of the event 14 g
3.
Credit for additional personnel 4.
Dependency of human actions 5.
Operator stress level Dependency Cut-off PRA Sensitivity Results Window of Vulnerability
 
PRA Discussion 1.
Treatment of 1XP failure 3/4 Failure of 1XP is an independent failure unrelated to the performance deficiency identified in the SDP 3/4 Instead of setting the event to 1.0 or TRUE, it should be based on the probability of an incorrect breaker setting 15 3/4 Per Duke Root Cause, this was a random failure of the technician to properly set the breaker 3/4 Inspections demonstrated that similar breakers were set properly 3/4 Interview with responsible technician supports the conclusion that this was an independent, random failure 3/4 Duke calculated failure rate is 3.0E-02 3/4 Considering this credit alone, revised CCDP would be 4.7E-07
 
PRA Discussion 2.
Timing of the event 3/4 Refer to drawing and timeline 3/4 Time to midloop is significantly longer than assumed in the initial evaluations by Duke and NRC 3/4 Operators have 100 minutes instead of the assumed 70 minutes 16 3/4 This should be classified as expansive time, changing the multiplier by a factor of 10 (0.1 to 0.01) 3/4 Considering this credit alone, revised CCDP would be 4.9E-06
 
PRA Discussion 17
 
PRA Discussion ONS LOI Event Timeline Event Midloop LP 96 Closed - Event Ends LP 21 Opened - Makeup Starts Operators Enter AP for LOI Operators Dispatched to Open LP 21 and Close LP 96 18 0
50 100 150 200 Time (minutes)
Draindown via Purification Relief Valve Heatup and Boiloff Core Damage Occurs
 
PRA Discussion 3.
Credit for additional personnel 3/4 Shared Control Room - two complete crews and supporting shift personnel including OSM and STA 3/4 In excess of 15 people including management and author of EOP and AP 19 3/4 SDP evaluation is dominated by failure to recognize the LOI, yet no credit is given for these additional experts 3/4 Modest credit directly reduces the calculated significance of the event 3/4 Considering this credit alone, revised CCDP would be low E-06 to mid E-06
 
PRA Discussion 4.
Dependency of Human Actions 3/4 Human errors and the evaluation of their interdependence drives the SDP conclusion 3/4 Subjective determination (contrary to the SDP goal to be objective) 20 3/4 Dominant cutset contains two human errors
 
Failure to diagnose event (cognitive)
 
Failure to inject when level reaches midloop (cognitive/execution) 3/4 Dependency is more accurately evaluated by splitting the second action into its two parts (cognitive and execution) 3/4 Considering this credit alone, revised CCDP would be 5.7E-06
 
PRA Discussion 5.
Operator stress level 3/4 A key input to determining the failure to diagnose the event 3/4 Power interruption was less than 2 seconds 3/4 Decreasing inventory was quickly and correctly recognized 3/4 Multiple alarms silenced within minutes 21 p
3/4 Ample time available to diagnose and mitigate (100 minutes to midloop) 3/4 Nominal stress is more appropriate 3/4 Considering this credit alone, revised CCDP would be approximately 1E-05
 
Dependency Cut-Off
 
Dependency Cut-off not used in actual SDP but can become important 3/4 SDP evaluation cites NUREG good practice which proposes a cap of 1E-05 3/4 If applied, findings analyzed via the Shutdown SDP (which is 22 HRA driven) will be Yellow - not a useful insight 3/4 Previous Shutdown SDP findings have been characterized by the NRC as Green or White 3/4 Draft Low Power/Shutdown ANS Standard does not specify a limit - no industry consensus
 
PRA Sensitivity Results Factor Discussion Revised CCDP for each issue Color Treatment of 1XP Failure of 1XP is a latent error independent of the performance deficiency 4.7E-07 Green Timing of Event
> 100 minutes available to Mid-Loop vs. 70 minutes 4.9E-06 White 23 Additional Personnel Additional personnel independent of the operating crew were available Low E-06 to Mid E-06 White Diagnosis and Action Dependencies Action component of HEP is not dependent on cognitive component 5.7E-06 White Operator Stress Stress levels normal versus high
~1E-05 White - Yellow
 
Window of Vulnerability Event significance is very dependent on when it occurred 3/4 Midloop operation -- Reduced time to core damage; SDP result may be an order of magnitude higher 3/4 Refueling canal flooded -- Increased time to core damage; SDP result may be an order of magnitude lower 24 y
g 3/4 Unit in No Mode -- Event would not occur 3/4 Not in backcharge alignment -- Event would not occur
 
PRA Overview/Conclusions SDP for Shutdown Events is very dependent on human error evaluation and stretches the capabilities of HRA Analysis Reasonable analysts can reach quantitative conclusions that differ by an order of magnitude Quantitative results should be balanced by qualitative factors 25 3/4 Multiple independent cues throughout the event 3/4 Additional sources of RCS makeup 3/4 All required equipment available 3/4 Adequate procedural guidance to mitigate the event 3/4 Ample time to respond 3/4 Additional personnel to respond to the event Dukes calculated CCDP for this event is approximately 3.8E-07
 
Root Causes and Corrective Actions Preston Gillespie Oconee Station Manager 26 Preston Gillespie, Oconee Station Manager
 
Root Causes and Corrective Actions Two separate root cause analyses were performed 3/4 Loss of backcharge source during AVR maintenance 3/4 1XP did not re-energize as expected Prompt, thorough and comprehensive actions implemented An independent Event Investigation Team was formed to 27 An independent Event Investigation Team was formed to 3/4 Validate/determine causes and contributing causes 3/4 Ensure appropriate corrective and enhancement actions The LOI event has been factored into the Oconee Recovery Plan
 
Root Causes and Corrective Actions Root Cause (Loss of Backcharge Source) 3/4 Failure to recognize an unanticipated system interaction between the AVR trip circuitry and the backcharge power path.
During the development and review of procedure IP/0/B/2005/001, preparers and reviewers did not recognize that interruption and restoration of control power to the AVR 28 that interruption and restoration of control power to the AVR would actuate the K31 relay. Thus, steps to isolate actuation of the K31 relay were not included Contributing Cause 3/4 Backcharging Procedure OP/1/A/1107/005 did not provide isolation from unnecessary trip signals
 
Root Causes and Corrective Actions Actions Taken or Planned (Loss of Backcharge Source) 3/4 Comprehensive action plan includes dozens of action items 3/4 AVR maintenance procedure IP/0/B/2005/001 placed on hold and later revised to appropriately address backcharge path 3/4 Reviewed work activities planned during backcharging and 29 rescheduled many to when unit auxiliaries are on the startup transformer 3/4 Reviewed outage-related first-use procedures for risk impact 3/4 OP/1,2,3/A/1107/005 revised to isolate unnecessary trips and ensure protected trains are adequate
 
Root Causes and Corrective Actions Actions Taken or Planned (Loss of Backcharge Source) 3/4 AP-26 revised to enhance existing mitigation strategies 3/4 Upgraded simulator to model RCS conditions during outage 3/4 Performed LOI assessment Established administrative controls similar to reduced inventory 30 controls prior to dropping RCS loops Blocked open AOVs in LPI purification loop Eliminated use of LPI purification when in reduced inventory 3/4 Plan to enhance Nuclear System Directives 403 and 703 3/4 Formally establish electrical work integration team
 
Root Causes and Corrective Actions Root Cause (1XP did not re-energize as expected) 3/4 Failure to follow procedure. During the last breaker PM (1EOC23), the breaker technician failed to restore the breaker setting to the as-found HI instantaneous setting Contributing Causes 31 3/4 Procedure did not have a place keeper nor did it require concurrent verification for the breaker setting 3/4 Additional outage loads increased inrush on the breaker above the LO trip setpoint (not an issue with breaker set to HI)
 
Root Causes and Corrective Actions Actions Taken or Planned (1XP issue) 3/4 Comprehensive action plan includes numerous actions 3/4 1XP-F3A breaker magnetic trip setting returned to HI 3/4 IP/0/A/3011/013A revised to include concurrent verification for breaker setting (extent of condition review planned) 32 3/4 Reviewed loads off 1XP and scheduling of associated transfer of power procedures to minimize risk 3/4 Reviewed MCC breaker settings for 600 Volt molded case normal and emergency feeder breakers 3/4 Plan to perform breaker coordination study
 
Closing Remarks Dave Baxter Oconee Site Vice President 33 Dave Baxter, Oconee Site Vice President
 
Closing Remarks We understand and accept the finding The circumstances that led to the unplanned LOI did not meet Duke expectations Operators promptly recognized the LOI, quickly silenced alarms, and entered the appropriate procedures 34 pp p
p There was adequate mitigation capability Ample time was available to diagnose and mitigate the event Dukes calculated CCDP for the actual event is ~ 3.8E-07
 
Closing Remarks Processes would not have prevented the event from occurring during periods of higher risk; however, additional controls would be in place to help recognize and mitigate the event Two root cause analyses were performed Prompt, thorough and comprehensive actions implemented 35 p,
g p
p An independent Event Investigation Team was formed to validate causes and contributing causes and ensure appropriate corrective and enhancement actions
 
Closing Remarks Duke clearly recognizes the vital safety function performed by DHR during shutdown conditions and the importance of proper outage management to reduce the likelihood and 36 p
p g
g consequences of shutdown events
 
Simplified LPI Purification Diagram 37}}

Latest revision as of 13:27, 14 January 2025

Regulatory Conference, Unanticipated Reduction in Unit 1, RCS Inventory During Shutdown Conditions
ML090300249
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Site: Oconee  Duke Energy icon.png
Issue date: 01/29/2009
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Download: ML090300249 (37)


Text

Oconee Nuclear Station Regulatory Conference U

ti i t d R d ti i

U it 1 1

Unanticipated Reduction in Unit 1 RCS Inventory During Shutdown Conditions NRC Region II Office Atlanta, Georgia January 22, 2009

Duke Participants Dave Baxter Oconee Site Vice President Preston Gillespie Oconee Station Manager Eddie Anderson Oconee Operations Superintendent Rich Freudenberger Oconee Safety Assurance Manager 2

g y

g Steve Nader Duke PRA Engineering Supervisor Bryan Carroll Duke PRA Engineer Graham Davenport Oconee Regulatory Compliance Manager Dave Coyle Oconee Operations Support Manager Bob Meixell Oconee Regulatory Compliance Engineer Jeff Thomas Duke Regulatory Compliance Manager

Agenda Opening Remarks Initial Plant Conditions Event Discussion PRA Discussion Root Causes and Corrective Actions 3

Root Causes and Corrective Actions Closing Remarks

Opening Remarks The circumstances that led to the unplanned Loss of Inventory (LOI) did not meet Duke expectations 3/4 Inadequate Automatic Voltage Regulator (AVR) maintenance procedure IP/0/B/2005/001 resulted in main generator lockout and slow transfer of power 4

3/4 Failure to follow IP/0/A/3011/013A resulted in an over-current trip of the 1XP emergency feeder breaker due to an improperly set instantaneous magnetic trip device Duke agrees that the inadequate AVR maintenance procedure constituted a performance deficiency and a finding

Opening Remarks Two root cause analyses were performed 3/4 Loss of backcharge source during AVR maintenance 3/4 1XP 600 volt AC system failed to re-energize as expected Prompt, thorough and comprehensive actions implemented An Event Investigation Team performed an independent 5

An Event Investigation Team performed an independent review of causal analyses and action plans The LOI event has been factored into the Oconee Recovery Plan

Opening Remarks During the event:

3/4 Reactor Coolant System (RCS) level never decreased to the reduced inventory level (3 feet below flange) 3/4 Event was quickly and correctly recognized and diagnosed 3/4 Operators quickly entered the appropriate procedures 3/4 RCS level was restored within 17 minutes 6

3/4 RCS level was restored within 17 minutes 3/4 There was no core damage, no offsite release, and containment integrity was not compromised Processes would not have prevented the event from occurring during periods of higher risk; however, additional controls would be in place to help recognize and mitigate the event There are key differences between Dukes risk analysis and the risk analysis performed by the NRC

Initial Plant Conditions Event Description 7

Eddie Anderson, Oconee Operations Superintendent

Initial Plant Conditions Day 4 of Unit 1 EOC24 Refueling Outage (April 15, 2008)

Reactor in Cold Shutdown (Mode 6), RV head detensioned but still in place, and the equipment hatch was closed RCS Conditions 3/4 RCS level 70 inches on LT-5 (84 inches is RV flange) 8 3/4 RCS level 70 inches on LT 5 (84 inches is RV flange) 3/4 RCS temperature 96 F 3/4 Low Pressure Injection (LPI) Trains A and B in service 3/4 LPI in normal shutdown purification mode

Initial Plant Conditions Additional sources of RCS makeup:

3/4 Borated Water Storage Tank (BWST; 360,000 gallons) 3/4 Bleed Holdup Tank (BHUT; 60,000 gallons)

Bleed Transfer Pump 1A available LPI Pump 1C available 9

HPI Trains 1A and 1B available Electrical power supplied by backcharged main transformer Alternate power from switchyard available through startup transformer All emergency power sources available First-time performance of Automatic Voltage Regulator (AVR) Maintenance Procedure IP/0/B/2005/001

Event Discussion Interruption and restoration of control power to AVR actuated the K31 relay that caused Main Generator Lockout As designed, a slow transfer of auxiliary power to startup transformer restored Decay Heat Removal (DHR) in ~ 2 seconds 10 MCC-1XP failed to re-energize as expected Certain Air Operated Valves on the purification loop failed closed due to loss of solenoid power from 1XP 3/4 Purification valves repositioning caused LPI Pump discharge pressure to lift purification relief valve

Event Discussion Approximate Timeline 1323 - Unit 1 momentary interruption of power (~ 2 seconds) 1324 - Operators immediately check LPI status, review activated Statalarms, silence alarms, determine RV level decreasing from computer trend 1325 - AP/1/A/1700/026 (Loss of DHR) entered due to decreasing RCS level 11 1326 - Operators determine normal makeup lost and dispatch NEOs to open 1LP-21 (BWST Supply to LPI)

- Operator dispatched to close 1LP-96 (Purification Isolation) 1338 - RCS level at ~ 54.5 on LT-5 (lowest level observed)

- 1LP-21 throttled open 1340 - RCS Level at ~ 72 on LT-5 (level restored) 1344 - 1LP-21 closed. 1LP-96 closed to isolate purification to stop loss of RCS inventory. Approximately 2000 gallons of RCS transferred to MWHUT

Event Discussion LOI event was promptly recognized by multiple operators from computer trends and mitigated. Level was restored within 17 minutes Operator stress levels did not impact event mitigation 3/4 DHR repowered automatically 3/4 Alarms silenced within minutes 3/4 Event and mitigation not complicated (only system in service was DHR) 12 Additional mitigating equipment available per Defense In Depth (DID) sheets and use was proceduralized 3/4 LPI Injection from BWST (2 trains/2 pumps) 3/4 HPI Injection from BWST (2 trains/2 pumps) 3/4 BWST inventory at 360,000 gallons Extensive oversight to assist control room operators Operators had > 180 minutes to recognize and mitigate the LOI prior to core damage

PRA Discussion Steve Nader PRA Engineering Supervisor 13 Steve Nader, PRA Engineering Supervisor

PRA Discussion The CCDP for this event is approximately 3.8E-07 The primary differences between Dukes risk analysis and the risk analysis performed by the NRC are 1.

Treatment of 1XP failure 2.

Timing of the event 14 g

3.

Credit for additional personnel 4.

Dependency of human actions 5.

Operator stress level Dependency Cut-off PRA Sensitivity Results Window of Vulnerability

PRA Discussion 1.

Treatment of 1XP failure 3/4 Failure of 1XP is an independent failure unrelated to the performance deficiency identified in the SDP 3/4 Instead of setting the event to 1.0 or TRUE, it should be based on the probability of an incorrect breaker setting 15 3/4 Per Duke Root Cause, this was a random failure of the technician to properly set the breaker 3/4 Inspections demonstrated that similar breakers were set properly 3/4 Interview with responsible technician supports the conclusion that this was an independent, random failure 3/4 Duke calculated failure rate is 3.0E-02 3/4 Considering this credit alone, revised CCDP would be 4.7E-07

PRA Discussion 2.

Timing of the event 3/4 Refer to drawing and timeline 3/4 Time to midloop is significantly longer than assumed in the initial evaluations by Duke and NRC 3/4 Operators have 100 minutes instead of the assumed 70 minutes 16 3/4 This should be classified as expansive time, changing the multiplier by a factor of 10 (0.1 to 0.01) 3/4 Considering this credit alone, revised CCDP would be 4.9E-06

PRA Discussion 17

PRA Discussion ONS LOI Event Timeline Event Midloop LP 96 Closed - Event Ends LP 21 Opened - Makeup Starts Operators Enter AP for LOI Operators Dispatched to Open LP 21 and Close LP 96 18 0

50 100 150 200 Time (minutes)

Draindown via Purification Relief Valve Heatup and Boiloff Core Damage Occurs

PRA Discussion 3.

Credit for additional personnel 3/4 Shared Control Room - two complete crews and supporting shift personnel including OSM and STA 3/4 In excess of 15 people including management and author of EOP and AP 19 3/4 SDP evaluation is dominated by failure to recognize the LOI, yet no credit is given for these additional experts 3/4 Modest credit directly reduces the calculated significance of the event 3/4 Considering this credit alone, revised CCDP would be low E-06 to mid E-06

PRA Discussion 4.

Dependency of Human Actions 3/4 Human errors and the evaluation of their interdependence drives the SDP conclusion 3/4 Subjective determination (contrary to the SDP goal to be objective) 20 3/4 Dominant cutset contains two human errors

Failure to diagnose event (cognitive)

Failure to inject when level reaches midloop (cognitive/execution) 3/4 Dependency is more accurately evaluated by splitting the second action into its two parts (cognitive and execution) 3/4 Considering this credit alone, revised CCDP would be 5.7E-06

PRA Discussion 5.

Operator stress level 3/4 A key input to determining the failure to diagnose the event 3/4 Power interruption was less than 2 seconds 3/4 Decreasing inventory was quickly and correctly recognized 3/4 Multiple alarms silenced within minutes 21 p

3/4 Ample time available to diagnose and mitigate (100 minutes to midloop) 3/4 Nominal stress is more appropriate 3/4 Considering this credit alone, revised CCDP would be approximately 1E-05

Dependency Cut-Off

Dependency Cut-off not used in actual SDP but can become important 3/4 SDP evaluation cites NUREG good practice which proposes a cap of 1E-05 3/4 If applied, findings analyzed via the Shutdown SDP (which is 22 HRA driven) will be Yellow - not a useful insight 3/4 Previous Shutdown SDP findings have been characterized by the NRC as Green or White 3/4 Draft Low Power/Shutdown ANS Standard does not specify a limit - no industry consensus

PRA Sensitivity Results Factor Discussion Revised CCDP for each issue Color Treatment of 1XP Failure of 1XP is a latent error independent of the performance deficiency 4.7E-07 Green Timing of Event

> 100 minutes available to Mid-Loop vs. 70 minutes 4.9E-06 White 23 Additional Personnel Additional personnel independent of the operating crew were available Low E-06 to Mid E-06 White Diagnosis and Action Dependencies Action component of HEP is not dependent on cognitive component 5.7E-06 White Operator Stress Stress levels normal versus high

~1E-05 White - Yellow

Window of Vulnerability Event significance is very dependent on when it occurred 3/4 Midloop operation -- Reduced time to core damage; SDP result may be an order of magnitude higher 3/4 Refueling canal flooded -- Increased time to core damage; SDP result may be an order of magnitude lower 24 y

g 3/4 Unit in No Mode -- Event would not occur 3/4 Not in backcharge alignment -- Event would not occur

PRA Overview/Conclusions SDP for Shutdown Events is very dependent on human error evaluation and stretches the capabilities of HRA Analysis Reasonable analysts can reach quantitative conclusions that differ by an order of magnitude Quantitative results should be balanced by qualitative factors 25 3/4 Multiple independent cues throughout the event 3/4 Additional sources of RCS makeup 3/4 All required equipment available 3/4 Adequate procedural guidance to mitigate the event 3/4 Ample time to respond 3/4 Additional personnel to respond to the event Dukes calculated CCDP for this event is approximately 3.8E-07

Root Causes and Corrective Actions Preston Gillespie Oconee Station Manager 26 Preston Gillespie, Oconee Station Manager

Root Causes and Corrective Actions Two separate root cause analyses were performed 3/4 Loss of backcharge source during AVR maintenance 3/4 1XP did not re-energize as expected Prompt, thorough and comprehensive actions implemented An independent Event Investigation Team was formed to 27 An independent Event Investigation Team was formed to 3/4 Validate/determine causes and contributing causes 3/4 Ensure appropriate corrective and enhancement actions The LOI event has been factored into the Oconee Recovery Plan

Root Causes and Corrective Actions Root Cause (Loss of Backcharge Source) 3/4 Failure to recognize an unanticipated system interaction between the AVR trip circuitry and the backcharge power path.

During the development and review of procedure IP/0/B/2005/001, preparers and reviewers did not recognize that interruption and restoration of control power to the AVR 28 that interruption and restoration of control power to the AVR would actuate the K31 relay. Thus, steps to isolate actuation of the K31 relay were not included Contributing Cause 3/4 Backcharging Procedure OP/1/A/1107/005 did not provide isolation from unnecessary trip signals

Root Causes and Corrective Actions Actions Taken or Planned (Loss of Backcharge Source) 3/4 Comprehensive action plan includes dozens of action items 3/4 AVR maintenance procedure IP/0/B/2005/001 placed on hold and later revised to appropriately address backcharge path 3/4 Reviewed work activities planned during backcharging and 29 rescheduled many to when unit auxiliaries are on the startup transformer 3/4 Reviewed outage-related first-use procedures for risk impact 3/4 OP/1,2,3/A/1107/005 revised to isolate unnecessary trips and ensure protected trains are adequate

Root Causes and Corrective Actions Actions Taken or Planned (Loss of Backcharge Source) 3/4 AP-26 revised to enhance existing mitigation strategies 3/4 Upgraded simulator to model RCS conditions during outage 3/4 Performed LOI assessment Established administrative controls similar to reduced inventory 30 controls prior to dropping RCS loops Blocked open AOVs in LPI purification loop Eliminated use of LPI purification when in reduced inventory 3/4 Plan to enhance Nuclear System Directives 403 and 703 3/4 Formally establish electrical work integration team

Root Causes and Corrective Actions Root Cause (1XP did not re-energize as expected) 3/4 Failure to follow procedure. During the last breaker PM (1EOC23), the breaker technician failed to restore the breaker setting to the as-found HI instantaneous setting Contributing Causes 31 3/4 Procedure did not have a place keeper nor did it require concurrent verification for the breaker setting 3/4 Additional outage loads increased inrush on the breaker above the LO trip setpoint (not an issue with breaker set to HI)

Root Causes and Corrective Actions Actions Taken or Planned (1XP issue) 3/4 Comprehensive action plan includes numerous actions 3/4 1XP-F3A breaker magnetic trip setting returned to HI 3/4 IP/0/A/3011/013A revised to include concurrent verification for breaker setting (extent of condition review planned) 32 3/4 Reviewed loads off 1XP and scheduling of associated transfer of power procedures to minimize risk 3/4 Reviewed MCC breaker settings for 600 Volt molded case normal and emergency feeder breakers 3/4 Plan to perform breaker coordination study

Closing Remarks Dave Baxter Oconee Site Vice President 33 Dave Baxter, Oconee Site Vice President

Closing Remarks We understand and accept the finding The circumstances that led to the unplanned LOI did not meet Duke expectations Operators promptly recognized the LOI, quickly silenced alarms, and entered the appropriate procedures 34 pp p

p There was adequate mitigation capability Ample time was available to diagnose and mitigate the event Dukes calculated CCDP for the actual event is ~ 3.8E-07

Closing Remarks Processes would not have prevented the event from occurring during periods of higher risk; however, additional controls would be in place to help recognize and mitigate the event Two root cause analyses were performed Prompt, thorough and comprehensive actions implemented 35 p,

g p

p An independent Event Investigation Team was formed to validate causes and contributing causes and ensure appropriate corrective and enhancement actions

Closing Remarks Duke clearly recognizes the vital safety function performed by DHR during shutdown conditions and the importance of proper outage management to reduce the likelihood and 36 p

p g

g consequences of shutdown events

Simplified LPI Purification Diagram 37