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{{Adams|number = ML092230096}}
{{Adams
| number = ML092240592
| issue date = 08/12/2009
| title = IR 05000247-09-003, on 04/01/2009 - 06/30/2009; Indian Point Nuclear Generating (Indian Point) Unit 2; Event Follow-up
| author name = Gray M
| author affiliation = NRC/RGN-I/DRP/PB2
| addressee name = Pollock J
| addressee affiliation = Entergy Nuclear Operations, Inc
| docket = 05000247
| license number = DPR-064
| contact person = Gray M
| case reference number = FOIA/PA-2010-0133, FOIA/PA-2011-0021
| document report number = IR-09-003
| document type = Inspection Report, Letter
| page count = 39
}}


{{IR-Nav| site = 05000247 | year = 2009 | report number = 003 }}
{{IR-Nav| site = 05000247 | year = 2009 | report number = 003 }}


=Text=
=Text=
{{#Wiki_filter: August 10, 2009 Mr. Joseph Site Vice President Entergy Nuclear Operations, Inc. Indian Point Energy Center 450 Broadway, GSB Buchanan, NY 10511-0249
{{#Wiki_filter:August 12, 2009


SUBJECT: INDIAN POINT NUCLEAR GENERATING UNIT 3 - NRC INTEGRATED INSPECTION REPORT 05000286/2009003
==SUBJECT:==
INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED INSPECTION REPORT 05000247/2009003


==Dear Mr. Pollock:==
==Dear Mr. Pollock:==
On June 30, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 3. The enclosed integrated inspection report documents the inspection results, which were discussed on July 22, 2009, with you and other members of your staff.
On June 30, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report documents the inspection results, which were discussed on July 22, 2009, with you and other members of your staff.


The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. This report documents two findings of very low safety significance (Green), one of which was also determined to be a violation of NRC requirements. However, because of the very low safety significance, and because the finding was entered into your corrective action program, the NRC is treating the finding as a non-cited violation (NCV), consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest this NCV, you should provide a written response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Indian Point Nuclear Generating Unit 3. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspectors at Indian Point Nuclear Generating Unit 3. The information you provide will be considered in accordance with Inspection Manual Chapter 0305. In accordance with Title 10 of the Code of Federal Regulations (10 CFR) Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of the Publicly Available Records System (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.


Sincerely,/RA/ Mel Gray, Chief Projects Branch 2 Division of Reactor Projects Docket No. 50-286 License No. DPR-64
This report documents one self-revealing finding of very low safety significance (Green).


===Enclosure:===
Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of its very low safety significance and because it is entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region 1; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region 1, and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.
Inspection Report No. 05000286/2009003 w/


===Attachment:===
In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Supplemental Information cc w/encl: Senior Vice President, Entergy Nuclear Operations Vice President, Operations, Entergy Nuclear Operations Vice President, Oversight, Entergy Nuclear Operations Senior Manager, Nuclear Safety and Licensing, Entergy Nuclear Operations Senior Vice President and COO, Entergy Nuclear Operations Assistant General Counsel, Entergy Nuclear Operations Manager, Licensing, Entergy Nuclear Operations C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law A. Donahue, Mayor, Village of Buchanan J. G. Testa, Mayor, City of Peekskill R. Albanese, Four County Coordinator S. Lousteau, Treasury Department, Entergy Services, Inc. Chairman, Standing Committee on Energy, NYS Assembly Chairman, Standing Committee on Environmental Conservation, NYS Assembly Chairman, Committee on Corporations, Authorities, and Commissions M. Slobodien, Director, Emergency Planning P. Eddy, NYS Department of Public Service Assemblywoman Sandra Galef, NYS Assembly T. Seckerson, County Clerk, Westchester County Board of Legislators A. Spano, Westchester County Executive R. Bondi, Putnam County Executive C. Vanderhoef, Rockland County Executive E. A. Diana, Orange County Executive T. Judson, Central NY Citizens Awareness Network M. Elie, Citizens Awareness Network Public Citizen's Critical Mass Energy Project M. Mariotte, Nuclear Information & Resources Service F. Zalcman, Pace Law School, Energy Project
 
Sincerely,
/RA/
 
Mel Gray, Chief
 
Projects Branch 2
 
Division of Reactor Projects
 
Docket No. 50-247 License No. DPR-26
 
Enclosure:
Inspection Report No. 05000247/2009003
 
w/ Attachment: Supplemental Information  
 
cc w/encl:
Senior Vice President, Entergy Nuclear Operations Vice President, Operations, Entergy Nuclear Operations Vice President, Oversight, Entergy Nuclear Operations Senior Manager, Nuclear Safety and Licensing, Entergy Nuclear Operations Senior Vice President and COO, Entergy Nuclear Operations Assistant General Counsel, Entergy Nuclear Operations Manager, Licensing, Entergy Nuclear Operations C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law A. Donahue, Mayor, Village of Buchanan J. G. Testa, Mayor, City of Peekskill R. Albanese, Four County Coordinator S. Lousteau, Treasury Department, Entergy Services, Inc.
 
Chairman, Standing Committee on Energy, NYS Assembly Chairman, Standing Committee on Environmental Conservation, NYS Assembly Chairman, Committee on Corporations, Authorities, and Commissions M. Slobodien, Director, Emergency Planning P. Eddy, NYS Department of Public Service Assemblywoman Sandra Galef, NYS Assembly T. Seckerson, County Clerk, Westchester County Board of Legislators A. Spano, Westchester County Executive R. Bondi, Putnam County Executive C. Vanderhoef, Rockland County Executive E. A. Diana, Orange County Executive T. Judson, Central NY Citizens Awareness Network M. Elie, Citizens Awareness Network Public Citizen's Critical Mass Energy Project M. Mariotte, Nuclear Information & Resources Service F. Zalcman, Pace Law School, Energy Project L. Puglisi, Supervisor, Town of Cortlandt Congressman John Hall Congresswoman Nita Lowey Senator Kirsten E. Gillibrand Senator Charles Schumer G. Shapiro, Senator Gillibrand 's Staff J. Riccio, Greenpeace P. Musegaas, Riverkeeper, Inc.
 
M. Kaplowitz, Chairman of County Environment & Health Committee A. Reynolds, Environmental Advocates D. Katz, Executive Director, Citizens Awareness Network K. Coplan, Pace Environmental Litigation Clinic M. Jacobs, IPSEC W. Little, Associate Attorney, NYSDEC M. J. Greene, Clearwater, Inc.
 
R. Christman, Manager Training and Development J. Spath, New York State Energy Research, SLO Designee F. Murray, President & CEO, New York State Energy Research A. J. Kremer, New York Affordable Reliable Electricity Alliance (NY AREA) ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,
/RA/
 
Mel Gray, Chief
 
Projects Branch 2
 
Division of Reactor Projects
 
Docket No. 50-286 License No. DPR-64
 
Enclosure:
Inspection Report No. 05000286/2009003
 
w/ Attachment: Supplemental Information
 
Distribution w/encl:
(via E-mail)
S. Collins, RA M. Dapas, DRA D. Lew, DRP J. Clifford, DRP L. Trocine, RI OEDO R. Nelson, NRR N. Salgado, NRR M. Kowal, NRR J. Boska, PM, NRR J. Hughey, NRR M. Gray, DRP B. Bickett, DRP S. McCarver, DRP P. Cataldo, SRI, IP3 D. Hochmuth, DRP D. Bearde, DRP ROPReportsResources@nrc.gov RI Docket Room (with concurrences
 
SUNSI Review Complete: __bab___(Reviewers Initial)
 
DOCUMENT NAME: G:\\DRP\\BRANCH2\\a - Indian Point 2\\Inspection Reports\\IP2 IR2009-003\\IP2 2009.003. r2.doc After declaring this document An Official Agency Record it will be released to the Public To Receive a copy of this document, indicate in the box: C = Copy without attachment/enclosure E = Copy with attachment/enclosure N = No copy
 
ML0922240592 Office RI/DRP
 
RI/DRP
 
RI/DRP
 
Name GMalone/bab for BBickett/bab MGray/mxg Date 07/31/09 08/05/09 08/12/09
 
OFFICAL AGENCY RECORD
 
Enclosure
 
U.S. Nuclear Regulatory Commission
 
Region I
 
Docket No.:
 
50-247
 
License No.:
DPR-26
 
Report No.:
 
05000247/2009003
 
Licensee:
 
Entergy Nuclear Northeast (Entergy)
 
Facility:
 
Indian Point Nuclear Generating Unit 2
 
Location:
 
450 Broadway, GSB
 
Buchanan, NY 10511-0249
 
Dates:
 
April 1, 2009 through June 30, 2009
 
Inspectors:
 
G. Malone, Senior Resident Inspector - Indian Point 2
 
C. Hott, Resident Inspector - Indian Point 2
 
D. Johnson, Physical Security Inspector
 
J. Noggle, Senior Health Physicist
 
S. McCarver, Project Engineer
 
E. Huang, Reactor Inspector
 
O. Ayegbusi, Reactor Inspector
 
Approved By:
Mel Gray, Chief
 
Projects Branch 2
 
Division of Reactor Projects
 
Enclosure


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
......................................................................................................... 3
IR 05000247/2009003; 04/01/2009 - 06/30/2009; Indian Point Nuclear Generating (Indian Point)
 
Unit 2; Event Follow-up.
 
This report covered a three-month period of inspection by resident and region based inspectors.
 
One finding of very low significance (Green) was identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
Significance Determination Process. The cross-cutting aspect for the finding was determined using IMC 0305, Operating Reactor Assessment Program. Findings for which the significance determination process (SDP) does not apply may be Green, or be assigned a severity level after NRC management review. The NRCs program for overseeing safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
 
===Cornerstone: Mitigating Systems===
*
: '''Green.'''
The inspectors documented a self-revealing finding of very low safety significance because Entergy engineers did not provide adequate guidance in a design change package for installation of tubing in the 21 main boiler feedwater pump (MBFP) control system that eventually led to the tubing failure and an unplanned trip of the reactor plant. Entergys design change procedure required that instructions delineating installation precautions be provided in the design change package. Entergys corrective actions included repairing the affected tubing, identifying and replacing similar tubing on the 22 MBFP, and examining Unit 3 MBFPs to identify the extent of the condition. Entergy staff placed this issue into the corrective action program and performed a root cause analysis.
 
The finding was more than minor because it was associated with the design control attribute of the Initiating Events cornerstone and affected its objective to limit the likelihood of events that affect plant stability and challenge critical safety functions during shutdown, as well as power operations. Specifically, the incorrectly installed MBFP control tubing resulted in a loss of the 21 MBFP and, ultimately, a reactor trip due to low steam generator water level.
 
The inspectors determined that the finding was of very low safety significance (Green) using the Phase 2 Indian Point Unit 2 risk-informed inspection notebook, in accordance with IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations.
 
The inspectors determined there was no cross-cutting issue associated with the finding because the performance deficiency did not reflect current licensee performance.
 
Specifically, the performance deficiency occurred several years ago and was outside the current assessment period, and procedures have since been improved in the design control, work control and vendor control processes that reduced the likelihood of vendors working on equipment without sufficient training or work instructions. (Section 4OA3)
 
===Other Findings===
* A violation of very low safety significance was identified by Entergy staff and has been reviewed by the inspectors. Corrective actions taken or planned by Entergy staff have been entered into Entergy's corrective action program. The violation and corrective action tracking number is listed in Section 4OA7 of this report.


=REPORT DETAILS=
=REPORT DETAILS=
===Summary of Plant Status===
Indian Point Unit 2 began the inspection period operating at full reactor power (100%). On April 3, 2009, Entergy operators manually shut down Unit 2 because of lowering water levels in the steam generators caused by the trip of a main boiler feed pump. Following investigation and repairs, operators initiated reactor start-up and the plant reached full power operation on April 5, 2009. The reactor trip and associated equipment issues are described further in Section 4OA3. Unit 2 remained at or near full power during the remainder of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
........................................................................................................... 5    1R01 Adverse Weather Protection .................................................................................... 5    1R04 Equipment Alignment .............................................................................................. 6    1R05 Fire Protection ......................................................................................................... 7    1R11 Licensed Operator Requalification Program ............................................................ 9    1R12 Maintenance Effectiveness ...................................................................................... 9    1R13 Maintenance Risk Assessments/Emergent Work Control ...................................... 10    1R15 Operability Evaluations .......................................................................................... 11    1R18 Plant Modifications ................................................................................................ 11    1R19 Post-Maintenance Testing ..................................................................................... 12    1R20 Refueling and Outage Activities............................................................................. 13    1R22 Surveillance Testing .............................................................................................. 14    1EP6 Drill Evaluation
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
 
{{a|1R01}}
 
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01|count=3}}
 
===.1 Summer Readiness of Offsite and Alternate AC Power Systems===
====a. Inspection Scope====
The inspectors verified that plant features and procedures for operation and continued availability of offsite and alternate AC power systems were appropriate. Specifically, the inspectors reviewed station procedures that describe roles, responsibilities, and actions related to the control of switching operations, emergency operations, and degraded conditions on the 13.8kV, 138kV, and 345kV electric power distribution system in the Buchanan Switchyard and onsite at Indian Point. Additionally, the inspectors walked down portions of the Buchanan Switchyard, onsite high voltage components, and the Appendix R diesel generator. The inspectors reviewed outstanding maintenance work orders and condition reports (CRs) related to these systems to verify Entergy personnel were appropriately prioritizing work and correcting problems in accordance with station procedures. Documents reviewed are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Station Readiness for Summer Heat Conditions===
====a. Inspection Scope====
The inspectors reviewed the readiness of risk-significant systems for summer hot weather conditions. The inspectors reviewed Entergys adverse weather procedures, operating experience, corrective action program, Updated Final Safety Analysis Report (UFSAR),
Technical Specifications (TS), operating procedures, staffing, and applicable plant documents to determine the types of adverse weather challenges to which the site is susceptible. The inspectors also checked local area temperatures, as well as the operability of ventilation and air conditioning cooling systems, to ensure the plant was prepared for warm weather conditions. In addition, the following risk-significant systems that were required to be protected from adverse weather conditions were selected and collectively represented one inspection sample:
* Main steam isolation system;
* 480-Volt system; and
* Appendix R emergency diesel generator system.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Emergent Heat Conditions on April 27-28, 2009===
====a. Inspection Scope====
The inspectors evaluated implementation of the adverse weather preparation procedures and compensatory measures before the onset of, and during adverse weather conditions.
 
Specifically, the inspectors evaluated Entergys preparations and compensatory measures taken during a period of hot weather from April 27 to April 28, 2009. The inspectors conducted walkdowns of plant equipment and reviewed operating procedures to ensure that equipment important to safety would not be adversely affected by severe weather conditions.
 
The documents reviewed during this inspection are listed in the Attachment. This inspection satisfied one inspection sample for the onset of adverse weather.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R04}}
 
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04Q|count=3}}
 
===.1 Partial System Walkdowns===
====a. Inspection Scope====
The inspectors performed partial system walkdowns to verify the operability of redundant or diverse trains and components during periods of system train unavailability or following periods of maintenance. The inspectors referenced system procedures, UFSAR, and system drawings to verify the alignment of the available train supported its required safety functions. The inspectors also reviewed applicable CRs and work orders to ensure Entergy personnel identified and properly addressed equipment discrepancies that could potentially impair the capability of the available train, as required by Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action. The documents reviewed during these inspections are listed in the Attachment.
 
The inspectors performed a partial walkdown on the following systems, which represented three inspection samples:
* 21 and 23 component cooling water pumps during maintenance on the 22 component cooling water pump;
* 22 containment spray pump system train when the 21 containment spray pump was tagged out for maintenance; and
* 21 charging pump during repairs to the 23 charging pump.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Full System Walkdown===
{{IP sample|IP=IP 71111.04S|count=1}}
 
====a. Inspection Scope====
The inspectors performed a complete system walkdown of accessible portions of the non-essential service water system to identify discrepancies between the existing equipment lineup and the required lineup. The inspectors reviewed operating procedures, surveillance tests, piping and instrumentation drawings, equipment lineup check-off lists, and the UFSAR to verify the system was aligned to perform its required safety functions. The inspectors reviewed a sample of CRs written to address deficiencies associated with the system to ensure they were appropriately evaluated and resolved. The documents reviewed during this inspection are listed in the Attachment. The walkdown of the non-essential service water system represented one inspection sample.
 
====b. Findings====
No findings of significance were identified. {{a|1R05}}
 
==1R05 Fire Protection
 
==
===.1 Resident Inspector Quarterly Walkdowns===
{{IP sample|IP=IP 71111.05Q|count=7}}
 
====a. Inspection Scope====
The inspectors conducted tours of several fire areas to assess the material condition and operational status of fire protection features. The inspectors verified, consistent with the applicable administrative procedures, that: combustibles and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with Entergys fire protection program. The inspectors evaluated the fire protection program for conformance with the requirements of License Condition 2.K. The documents reviewed during this inspection are listed in the Attachment. This inspection represented seven inspection samples for fire protection tours, and was conducted in the following areas:
* Fire Zone 5, 21 charging pump room;
* Fire Zone 6, 22 charging pump room;
* Fire Zone 7, 23 charging pump room;
* Fire Zone 1A, containment piping penetration room;
* Fire Zone 1, component cooling pump room;
* Fire Zone 11, cable spreading room; and
* Fire Zone 66A, service water valve and strainer pit.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Annual Fire Drill Sample===
====a. Inspection Scope====
The inspectors observed the fire brigades response to an actual fire alarm on May 18, 2009.
 
The fire brigade was dispatched to a manhole inside the protected area containing 138kV offsite power cables used to allow power to be cross-connected between Unit 2 and Unit 3 138kV switchyards. The inspectors verified the fire brigade responded to the call in a timely manner, protective clothing and turnout gear was properly worn, appropriate fire fighting equipment was selected and made ready for use, and the fire brigade leader exhibited command-and-control of the scene.
 
====b. Findings====
No findings of significance were identified. The heat and smoke identified in the manhole were due to an electrical fault in the three-phase non-safety related power cables in the vault. Protection relays in the electrical system automatically isolated the fault from the rest of the 138kV switchyard following the fault. There was no other equipment in the manhole and no extinguishing material was required to be discharged.
 
{{a|1R06}}
 
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06|count=1}}
 
====a. Inspection Scope====
The inspectors completed one internal flood protection sample. The inspectors reviewed selected risk-important plant design features and Entergy procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors focused on mitigation strategies and equipment for the 15 elevation of the auxiliary feed pump building, including the 21, 22, and 23 auxiliary boiler feed pump areas. The inspectors reviewed flood analysis and design documents, including the UFSAR, engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis.
 
====b. Findings====
No findings of significance were identified. {{a|1R11}}
 
==1R11 Licensed Operator Requalification Program
 
==
===.1 Quarterly Review===
{{IP sample|IP=IP 71111.11Q|count=1}}
 
====a. Inspection Scope====
On June 10, 2009, the inspectors observed licensed operator simulator training, which included an anticipated transient without a scram and a loss of primary coolant scenario, to verify operator performance was adequate and evaluators were identifying and documenting crew performance problems. The inspectors evaluated the performance of risk-significant operator actions including the use of emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms, performance of timely control board operation and manipulation, and the oversight and direction provided by the control room supervisor. The inspectors also assessed simulator fidelity with respect to the actual plant. The inspectors evaluated licensed operator training for conformance with the requirements of 10 CFR Part 55, Operator Licenses. The documents reviewed during this inspection are listed in the
. This observation of operator simulator training represented one inspection sample.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R12}}
 
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12Q|count=2}}
 
====a. Inspection Scope====
The inspectors reviewed performance-based problems that involved structures, systems, and components (SSCs) to assess the effectiveness of maintenance activities.
 
When applicable, the reviews focused on:
* Proper maintenance rule scoping in accordance with 10 CFR 50.65;
* Characterization of reliability issues;
* Changing system and component unavailability;
* 10 CFR 50.65(a)(1) and (a)(2) classifications;
* Identifying and addressing common cause failures;
* Trending of system flow and temperature values;
* Appropriateness of performance criteria for SSCs classified (a)(2); and
* Adequacy of goals and corrective actions for SSCs classified (a)(1).
 
The inspectors also reviewed system health reports, maintenance backlogs, and maintenance rule basis documents. The inspectors evaluated maintenance effectiveness and monitoring activities against the requirements of 10 CFR 50.65. The documents reviewed during this inspection are listed in the Attachment. The following samples were reviewed and represented two inspection samples:
* Primary water make-up system; and
* 22 service water pump bearing failures.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=9}}
 
====a. Inspection Scope====
The inspectors reviewed scheduled and emergent maintenance activities to verify that the appropriate risk assessments were performed prior to removing equipment from service for maintenance or repair. The inspectors reviewed selected risk assessments to verify assessments were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent work was performed, the inspectors reviewed the plant risk to ensure risk was promptly reassessed and managed. Documents reviewed during this inspection are listed in the Attachment. The following activities represented nine inspection samples:
* Planned maintenance on residual heat removal system valve during safety injection system venting;
* Steam generator steam flow testing during emergent work on a turbine hall cooling pump and 23 control rod drive mechanism fan;
* Planned maintenance on 22 auxiliary boiler feed pump during undervoltage relay replacement;
* Planned maintenance on 96951 138kV feeder line during 21 safety injection pump and valve testing;
* Planned maintenance on 21 primary water pump, 22 service water pump, 22 component cooling water pump, and the 96952 138kV feeder line;
* Planned maintenance activities during the week the 138kV cross-tie feeder line 33332 experienced a fault to ground and remained out of service;
* Emergent work on 22 circulating water pump and 23 containment fan coil unit with the 138kV cross-tie feeder line 33332, 21 primary water pump and valve FCV-110A out of service for maintenance;
* Emergent work activities associated with the 345kV breakers 7 and 11 (line 95891)with the 138kV line 33332 and 21 primary water pump out of service; and
* Emergent work activities associated with the 23 charging pump, 22 stator water cooling pump, and trip of the 23 motor control center.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R15}}
 
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15|count=7}}
 
===.1 Resident Quarterly Review===
====a. Inspection Scope====
The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications (TS). The inspectors reviews included verification that operability determinations were performed in accordance with procedure ENN-OP-104, Operability Determinations. The inspectors assessed the technical adequacy of the evaluations to ensure consistency with the TS, UFSAR, and associated design basis documents (DBDs). The documents reviewed are listed in the Attachment.
 
The following operability evaluations were reviewed and represented seven inspection
 
samples:
* 22 auxiliary boiler feed pump (ABFP) bearing conditions;
* Main steam isolation valve operability based on high ambient temperatures in the auxiliary feed pump building;
* 22 ABFP steam admission valve leak-by (PCV-1139);
* Residual heat removal pumps oil level deviations;
* Seismic qualification of vital 480V manholes;
* Seismic qualification of service water piping located at the intake structure (missing pipe support); and
* Leak in the 24 service water train discharge piping.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R18}}
 
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18|count=3}}
 
===.1 Temporary Modifications===
====a. Inspection Scope====
The inspectors reviewed three conditions as temporary plant modifications. The inspectors reviewed Entergys temporary modification procedure to verify that modifications were processed adequately. The inspectors verified the design bases, licensing bases, and performance capability of the system was not degraded by the temporary modification. In addition, the inspectors interviewed plant staff and reviewed issues entered into the corrective action program to determine whether Entergy had been effective in identifying and resolving problems associated with the temporary modifications. The documents reviewed are listed in the Attachment. The review of these temporary modifications represented three inspection samples. The following modifications were reviewed:
* Diagnostic equipment stationed external to 21 and 22 static inverters to troubleshoot intermittent inverter alarms and power supply swaps;
* Diagnostic equipment attached to a control room panel to troubleshoot intermittent grounds on the 21 battery charger; and
* 21 reactor coolant pump oil fill connection to allow remote filling of bearing reservoirs due to leakage.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R19}}
 
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=3}}
 
====a. Inspection Scope====
The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems, and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and
 
engineering personnel. The inspectors verified that: test acceptance criteria were clear and the test demonstrated operational readiness consistent with design basis documentation; test instrumentation had current calibrations with the appropriate range and accuracy for the application; and the tests were performed as written, with applicable prerequisites satisfied.
 
Upon completion of the tests, the inspectors reviewed whether equipment was returned to the proper alignment necessary to perform its safety function. Post-maintenance testing was evaluated against the requirements of 10 CFR 50, Appendix B, Criterion XI, Test Control.
 
The documents reviewed are listed in the Attachment. The following post-maintenance activities were reviewed and represented three inspection samples:
* Replacement of service water vacuum breaker valve SWN-9;
* Calibration and replacement of undervoltage relays 27-52 and 27-53 on bus 5A; and
* Post-maintenance test associated with the 2-year overhaul of the 28 service water traveling water screen.
 
====b. Findings====
No findings of significance were identified.
 
{{a|1R22}}
 
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=5}}
 
====a. Inspection Scope====
The inspectors observed performance of portions of surveillance tests and/or reviewed test data for selected risk-significant SSCs to assess whether tests satisfied TS, UFSAR, Technical Requirements Manual, and Entergy procedure requirements. The inspectors verified that: test acceptance criteria were clear, demonstrated operational readiness, and were consistent with design basis documentation; test instrumentation had accurate calibration, and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Following the tests, the inspectors verified that the equipment was capable of performing the required safety functions. The inspectors evaluated the surveillance tests against the requirements in TS.
 
The documents reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented five inspection samples:
* 2-PT-Q38, primary water storage tank level;
* 2-PT-M108, safety injection system venting;
* 2-PT-Q030C, 23 component cooling water pump in-service test;
* 2-PT-Q59, containment pressure bistables; and
* 2-PT-Q029B, 22 safety injection pump.
 
====b. Findings====
No findings of significance were identified.


==RADIATION SAFETY==
==RADIATION SAFETY==
....................................................................................................... 15    2PS2 Radioactive Materials Processing and Shipping
===Cornerstone: Public Radiation Safety (PS)===
2PS2 Radioactive Materials Processing and Shipping (71122.02 - 6 samples)
 
====a. Inspection Scope====
From June 22 to June 26, 2009, the inspectors conducted the following activities to verify that Entegy=s radioactive material processing and transportation programs complied with the requirements of 10 CFR 20, 61, and 71; and Department of Transportation (DOT) regulations 49 CFR 170-189.
: (1) The inspectors reviewed the solid radioactive waste system description in the UFSAR, the 2008 radiological effluent release report for information on the types and amounts of radioactive waste disposed, and the scope of the licensee=s audit program to verify that it meets the requirements of 10 CFR 20.1101.
: (2) The inspectors walked-down the liquid and solid radioactive waste processing systems to verify and assess that the current system configuration and operation agree with the descriptions contained in the UFSAR and in the Process Control Program (PCP); and reviewed the status of radioactive waste process equipment that is not operational and/or is abandoned in place; verified changes were reviewed and documented in accordance with 10 CFR 50.59, as appropriate. The inspectors reviewed the current processes for transferring and dewatering of radioactive waste resin and sludge discharges into shipping/disposal containers to determine if appropriate waste stream mixing and/or sampling procedures, and methodology for waste concentration averaging provide representative samples of the waste product for the purposes of waste classification as specified in 10CFR 61.55 for waste disposal.
: (3) The inspectors reviewed the radio-chemical sample analysis results for the licensee=s radioactive waste streams, reviewed the licensee=s use of scaling factors and calculations with respect to these radioactive waste streams to account for difficult-to-measure radionuclides, verified the licensee=s program assures compliance with 10 CFR 61.55 and 10 CFR 61.56 as required by Appendix G of 10 CFR 20, and reviewed Entergys program to ensure the waste stream composition data accounts for changing operational parameters and thus remains valid between the annual or biennial sample analysis update.
: (4) From June 24 to June 25, 2009, Entergy personnel prepared, packaged, and completed shipment No. 09-109 containing spent filters in a Type A cask for shipment to a waste processor. The inspectors observed the shipment preparations that included: packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifests, shipping papers provided to the driver, and licensee verification of shipment readiness.
: (5) The inspectors sampled the following non-excepted package shipment records and reviewed these records for compliance with NRC and DOT requirements:
 
$
08-055, spent fuel pool demineralizers shipment to a waste processor on April 7, 2008;
$
08-093, Hudson River silt shipment to a waste processor on May 15, 2008;
$
08-170, sodium hydroxide shipment to a waste processor on September 4, 2008;
$
08-200, Unit 1 debris shipment to a waste processor on November 4, 2008;
$
08-223, fuel sipping equipment shipment to Westinghouse on December 15, 2008;
$
09-068, dry active waste shipment to a waste processor on April 15, 2009;
$
09-100, Unit 1 pool sludge shipment to a waste processor on June 10, 2009;
$
09-102, Unit 2 primary resin shipment to a waste processor on June 17, 2009;
$
09-103, Unit 3 bead resin shipment to a waste processor on June 17, 2009; and
$
09-109, spent filter shipment to a waste processor on June 25, 2009.
: (6) The inspectors reviewed Entergy=s Licensee Event Reports, Special Reports, audits, State agency reports, and self-assessments for Indian Point Unit 2 related to the radioactive material and transportation programs performed since the last inspection to determine if identified problems are entered into the corrective action program for resolution. The inspectors also reviewed corrective action reports written against the radioactive material and shipping programs since the previous inspection.
 
====b. Findings====
No findings of significance were identified.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
......................................................................................................... 16   
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification ......................................................................... 16==


{{a|4OA2}}
==4OA1 Performance Indicator Verification==
==4OA2 Identification and Resolution of Problems .............................................................. 17==
{{IP sample|IP=IP 71151|count=3}}
 
====a. Inspection Scope====
The inspectors reviewed performance indicator data for the cornerstones listed below and used Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, to verify individual performance indicator accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment.
 
Initiating Events Cornerstone
* Unplanned Scrams with Complications
 
Mitigating Systems Cornerstone
* Safety System Functional Failures; and
* Emergency AC Power System Mitigating Systems Performance Indicator.
 
====b. Findings====
No findings of significance were identified.
 
{{a|4OA2}}
 
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152|count=5}}
 
===.1 a.===
Inspection Scope
 
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergys corrective action program. The review was accomplished by accessing Entergys computerized database for CRs and attending condition report group screening meetings.
 
In accordance with the baseline inspection modules, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for further follow-up and review. The inspectors assessed Entergy personnels threshold for problem identification, adequacy of the causal analysis, extent of condition reviews, and operability determinations, and timeliness of the associated corrective actions.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Annual Sample: Review of Corrective Actions Related to the Installation and Project===
Management of the New Alert and Notification System (ANS) (71152 - 1 sample)
 
====a. Inspection Scope====
The inspectors reviewed Entergy staff=s actions in response to CRs generated as a result of issues associated with the installation and project management of the new alert and notification system (ANS) for the Indian Point Energy Center. The inspectors reviewed Entergy procedures on project management and external stakeholder communications. In addition, the inspectors interviewed applicable members of Entergys staff including a lead project manager and licensing staff. The focus of this inspection was to verify that the corrective actions, reviewed during the December 2008 Enforcement Follow-up Inspection (Inspection Procedure 92702, NRC Inspection Report 50-247/286, 2008-503, dated January 27, 2009), were being completed in a thorough and timely manner.
 
====b. Findings====
& Observations
 
No findings of significance were identified. The inspectors reviewed CRs documenting issues related to the installation and project management of the new ANS placed into service for the Indian Point Energy Center in 2008. The inspectors determined Entergy personnel implemented or generated plans for appropriate corrective actions to address each issue that was identified. Additionally, the inspectors verified that Entergy staff appropriately implemented or generated plans for corrective actions to revise the project management process, require greater senior management oversight for projects, and develop a new procedure for interactions with external stakeholders.
 
===.3 Annual Sample: Station Auxiliary Transformer Tap Changer Alarms===
{{IP sample|IP=IP 71152|count=1}}
 
====a. Inspection Scope====
The inspectors reviewed Entergy staffs evaluations and corrective actions associated with the station auxiliary transformer tap changer hang-up alarms. Entergy staffs evaluations determined that for the tap changer alarm to occur: the tap changer is either in-between taps and a time delay of 12 seconds has passed; or the tap changer is greater than or equal to 16 taps in the raise or lower direction and a time delay of 12 seconds has passed. The alarm could also occur if there is a problem with the alarm circuitry. The inspectors reviewed Entergy staffs corrective actions to ensure that appropriate evaluations were performed and corrective actions were specified and prioritized. The inspectors also reviewed the follow-up actions to verify that the corrective actions identified were implemented.
 
====b. Findings====
& Observations
 
No findings of significance were identified.
 
The inspectors determined Entergys corrective action associated with the station auxiliary transformer tap changer hang-up alarms was appropriate. Entergys corrective actions in 2007 were to examine the alarm circuitry in addition to the scheduled preventive maintenance in the refueling outage of 2008. The inspectors noted that the 2008 preventive maintenance that was performed provided satisfactory results; however, the alarm issue continued to occur following the outage. Entergy personnel currently respond to the alarms by entering the appropriate alarm response procedure and TS 3.8.1 action statement each time the alarm occurs as well as manually verifying that the tap changer remained functional.
 
Entergy personnel are currently tracking and trending the alarms and plan to adjust the cam rollers of the tap changer in the spring outage of 2010. From the data of the last two alarms, Entergy staff indicated the two cam switches that communicate between the alarm circuit and the motor are not synchronized and an adjustment of the cam rollers should resolve the alarms. The inspectors determined that previous surveillance tests demonstrated the alarm circuitry is operable and the alarm will actuate on a valid signal. The inspectors determined the alarms appear to be an alarm issue only not an actual tap changer performance problem at this time. The inspectors determined the tap changer is able to perform its required function and corrective actions in place by Entergy personnel are adequate and commensurate with the risk significance of the issue.
 
===.4 Annual Sample: Review of Service Water Pump Motor Termination Failure (71152 - 1===
sample)
 
====a. Inspection Scope====
The inspectors selected CR-IP2-2008-00414 as a problem identification and resolution (PI&R) sample for a detailed follow-up review. CR-IP2-2008-00414 documented a failure of the 21 service water pump (SWP) motor B phase termination that resulted in the pump being declared inoperable on January 24, 2008. Entergy personnel determined the failure was due to the installation of an undersized cable termination lug during the previous replacement of the 21 SWP motor in April 2005. The inspectors assessed Entergy staffs problem identification threshold, apparent cause evaluation, extent of condition review, and the prioritization and timeliness of corrective actions to determine whether personnel were appropriately identifying, characterizing, and correcting problems associated with this issue and whether the planned or completed corrective actions were appropriate.
 
====b. Findings and Observations====
No findings of significance were identified.
 
The inspectors determined Entergy personnel adequately implemented its corrective action process regarding the initial discovery of the above issue. The CR packages were complete and included an apparent cause evaluation, extent of condition reviews, completed and planned corrective actions. Additionally, the elements of the CR packages were detailed and thorough. Specifically, the inspectors noted Entergy personnel implemented a new procedure for installing electric motor terminations EN-425-TER, Installation of Electric Motor Terminations. Also, Entergy trainers provided refresher training on performing electric motor terminations to the maintenance department and revised the electricians lesson plan EMF-EWS-01, Electrical Workmanship Standards to include training on electric motor terminations and scheduled the installation of infrared windows on the motor termination box for periodic thermography inspections. In addition, Entergy personnel revised 2-PMP-004-SWS, IP2 Service Water Pump and Motor Replacement Procedure, to use EN-425-TER for installing electrical motor terminations. As part of the extent of condition, Entergy staff performed detailed visual and thermography inspections of a selection of motor terminations. The inspectors determined the anomalies found during those inspections were adequately addressed.
 
During the inspection, the inspectors noted that the new procedure, EN-425-TER, was in a reserved status and the CR was closed indicating all corrective actions were completed.
 
Entergy staff overlooked activating EN-425-TER because 2-PMP-004-SWS had not been revised to reference the new procedure for installing electric motor terminations. The inspectors determined the issue was of minor significance because ENN-EE-S-008-IP had been revised to perform the same function as EN-425-TER and was available for use.
 
Following discussions with the inspectors, Entergy staff activated EN-425-TER and revised 2-PMP-004-SWS accordingly. The inspectors determined the corrective actions were timely and appeared appropriate to resolve the above issue. The inspectors determined these corrective actions addressed immediate equipment concerns as well as the extent of condition of the problem. In addition, the inspectors determined that adequate tracking mechanisms were in place to ensure scheduled corrective actions should be completed.
 
===.5 Annual Sample: Review of Root Cause Analysis and Actions Addressing the Underground===
Pipe Leak to the Condensate Storage Tank Return Line (71152 - 1 sample)
 
====a. Inspection Scope====
The inspectors reviewed Entergy staffs root cause analysis (RCA) for a leak in a section of underground return piping to the condensate storage tank (CST) that was identified on February 15, 2009. The inspectors reviewed the report and pertinent documents and interviewed station personnel to determine if the RCA adequately identified the causes of the leak, considered the extent of the problem, and provided for adequate corrective actions.
 
Background
 
On February 15, 2009, at approximately 3:00 p.m., an operator on rounds observed water in the CST return pipe sleeve where the pipe enters the auxiliary feed pump building floor.
 
Entergy staff took chemistry samples of the water and subsequently determined that 54 parts per billion (ppb) hydrazine was present, indicating that the water was likely from the condensate system. At 1:30 a.m. on February 16, operators declared the CST inoperable.
 
By February 18, Entergy staff determined the leak rate from the CST was approximately 17 gallons per minute (gpm), commenced excavation of the probable leak location, and confirmed that the leakage was from the CST return piping. On February 19, the excavation of the CST piping exposed the leak on the CST return pipe. Entergy technicians removed the pipe coating from the surrounding areas and performed ultrasonic testing of the pipe walls and determined the removed pipe was structurally sound and the metal loss was localized to the area of the pipe coating degradation. In addition to the hole identified in the horizontal run of the return pipe, Entergy staff discovered areas of minor metal loss on a pipe elbow in the same line due to pipe coating degradation. Entergy personnel removed the damaged section of piping and elbow and welded a new pipe portion in place on February 20. The CST was declared operable at 6:56 a.m. on February 21.
 
Entergy staff performed a RCA to determine the causes of the CST pipe leak. Entergy staff also contracted a vendor to analyze the portion of piping that was removed to determine the failure mode mechanisms. During excavation, Entergy staff identified a portion of the pipe backfill contained rocks ranging in size from 3 to 8 inches. Entergy staff reviewed the backfill specifications used during plant construction and determined the specifications did not provide detailed information on what size rocks could be present in this area. Entergy staff determined this particular area had a concrete slab poured on top of the fill and the slab was not intended to be a load bearing surface and, therefore, was not specific in requirements for the type of fill to be used. The vendor analysis of the pipe concluded that the leak was caused by external corrosion in areas where the pipe coating was degraded. Although the exact type of external corrosion could not be definitively concluded, Entergy staff determined the corrosion was likely the result of exposure to a range of ground water characteristics, and/or microbiologically influenced corrosion. Entergys RCA documented that the large rocks found in the backfill likely damaged the pipe coating during installation of the pipe and allowed the corrosion mechanisms described above to act on the localized metal surfaces.
 
Entergy staff determined the pipes were found to be in good condition where the coating was intact.
 
Entergys root cause team examined the stations capability to track water usage to determine whether it was reasonable for staff to identify the leakage prior to February 15.
 
The root cause team determined that it was not feasible for operators to detect the leakage from main condenser hotwell level indications or CST level indications because the rate of leakage (10-17gpm) was too small to detect considering the tank volumes and installed instrumentation. Furthermore, the root cause team supported its conclusion because several sources contribute to normal losses of inventory in the hotwell and require replenishment from the CST such as steam generator blowdown, non-safety auxiliary steam heating, and typical leakage from the non-safety related condensate system. Additionally, control room operators periodically monitor the decrease in CST level and make-up to the CST as necessary to ensure the CST level is maintained within required limits.
 
Entergys root cause team developed a corrective action plan to address the root and contributing causes of the pipe degradation. As part of those corrective actions, Entergy staff identified additional buried pipe inspections at several locations based on similar corrosion susceptibilities. Specifically, the root cause documentation described the Indian Point Buried Piping and Tank Inspection Program that has been under development since 2007, as part of a corporate-wide initiative to develop these programs at all Entergy sites.
 
The program identifies underground pipes at the site and assigns an impact assessment level based on safety impact of a failure. The high impact systems are also corrosion risk assessed by considering soil conditions, pipe material, and existing coatings or cathodic protection. The scheduling of examination of the pipes is determined by the potential safety impact and corrosion risk assessments. The non-destructive examinations may involve the use of guided wave technology, excavation and visual inspection, or other appropriate techniques as determined by Entergy personnel. Entergy managers plan to have the buried piping program fully developed by the end of 2009.
 
Entergys corrective action plan included the following actions listed below:
* Update the buried piping backfill and excavation specification;
* Implement improved inspection techniques for buried piping;
* Evaluate the need for cathodic protection systems and draining systems for select buried piping;
* Evaluate the use of existing monitoring wells for buried pipe and tank leaks for early detection capability;
* Conduct non-destructive examinations of the following pipe sections in the near term for investigation:
o CST return line (2 different locations)o CST supply line (2 different locations)o Service water line 408 (2 different locations); and
* Remainder of underground piping to be inspected in accordance with Buried Piping Program schedule.
 
As further background, by letter dated July 27, 2009, as clarified by letter dated August 6, 2009, Entergy management submitted an amendment to their license renewal application which modified the Indian Point Buried Piping and Tanks Inspection Program. This amendment reflected Entergys operating experience with the CST buried pipe leak at Unit 2 and included identification of additional buried pipe examinations. These non-destructive examinations will be performed by Entergy personnel at Units 2 and 3 prior to entering the period of extended operation and will supplement the six additional inspections referenced above.
 
====b. Findings and Observations====
No findings of significance were identified.
 
Overall, the inspectors reviewed Entergy staff activities related to the CST return line leak and the associated RCA and determined that Entergys staff identified the likely causes of the leak, considered the extent of the problem, and planned or provided for adequate corrective actions. Additionally, the inspectors concluded that Entergys root cause team adequately considered prior opportunities for identifying the CST return line leak.
 
The inspectors independently reviewed plant drawings and the backfill specifications provided by the engineer/architect at the time of plant construction and determined the drawings and specification did not detail or place limits on the type of backfill required and specifically did not prohibit rocks from being used in the backfill.
 
The inspectors noted that Entergy personnel performed required testing in accordance with the American Society of Mechanical Engineers Boiler & Pressure Vessel (ASME BPV) Code Section XI and 10 CFR 50.55a. ASME Section XI requires pipes similar to the CST return line be tested three times over the 10-year inspection interval by a pressure drop or flow test.
 
The inspectors determined that Entergy had procedures in place to implement ASME Code requirements for testing the subject CST retun line piping.
 
The inspectors considered whether the RCA evaluated the potential for Entergy personnel to identify the pipe leak prior to February 15, 2009. The inspectors concluded that Entergys RCA adequately considered prior opportunities for Entergy staff to identify the leak and that Entergy staff identified the leak when reasonable to do so. However, the inspectors identified two examples in which the RCA did not consider corrective actions that might aid Entergy staff in the early identification of leaks in the future should they occur.
* Entergys RCA evaluated Unit 2 CST level losses and condensate flow paths prior to February 2009 with a focus on the operators ability to identify secondary level changes that would be indicative of a CST leak. The root cause team concluded it would not be reasonable for operators to identify a secondary leak of 10-20 gpm on the Unit 2 CST using the installed instrumentation because the leak was very small compared to the large volume of the CST. While the RCA considered the CST volume and water usage flow paths, the inspectors determined the RCA did not consider or document an evaluation with respect to existing daily operational logs that could provide trend information on overall processed monthly water usage and make-up to the Unit 1 CST.
 
The inspectors review identified that operations personnel log the processed water sent from the stations on-site city water system to the Unit 1 CST such that the amount of water used daily by secondary plant operations on Unit 2 can be trended. The inspectors review of water usage identified a noticeable increase in water consumed by Unit 2 in November 2008 with a continued increase through February 2009 compared to typical water usage in prior years during the same months. When interviewed by inspectors, Entergy staff explained the log reading is used to verify station billing from the water conditioning vendor and not intended to be trended and tracked for purposes of Unit 2 CST water usage.
 
The inspectors determined it was not reasonable for Entergy staff to have identified the CST return pipe leak based on the increased water usage as logged for billing purposes considering there was not a prior history of CST pipe leaks. However, the inspectors review determined Entergys RCA did not document its evaluation of the capability to trend logged water usage data from year to year. Additionally, Entergys RCA did not evaluate whether this water usage data could be useful, in concert with other monitoring activities, to identify indications of potential leaks in the future as early as reasonably possible, whether they occur from safety related or non-safety related components.
* Entergys RCA reviewed previous inspection results for excavation of two sections of CST piping that were conducted by Entergy staff in October and November 2008 in response to recommendations from an Independent Safety Evaluation Report dated July 31, 2008. The excavated areas were located in areas between the CST and the auxiliary feed pump building. At that time, Entergy staff identified, based on non-destructive examinations, five areas of piping that required coating repair due to missing or damaged pipe coating. The inspectors review of Entergys examinations noted that the pipe walls at those locations in 2008 remained at or near their original manufactured thickness.
 
Based on observations and repairs made, Entergys staff concluded the pipes did not exhibit pipe degradation that would warrant further inspection of these same locations in the future. Additionally, the inspectors noted Entergys RCA described that during the 2008 excavations, Entergy staff observed water visible in a CST return line pipe collar where the piping entered the auxiliary feed pump building. Entergy staff performed chemistry analysis of this water and concluded, based on the sample results, that the pH, tritium levels, and absence of hydrazine indicated the leakage was consistent with groundwater chemistry during a time of heavy rains and was not indicative of CST water chemistry.
 
The inspectors concluded Entergy staff adequately assessed conditions surrounding the 2008 excavations. However, the inspectors determined the RCA did not evaluate the water present in the CST return pipe collar in October 2008 specific to the issue not being entered into the corrective action program. The inspectors determined it would have been appropriate for the RCA to evaluate whether corrective actions were appropriate to reinforce the expectations for staff to enter unanticipated visual indications of water in the CST pipe return floor collar within the corrective action program to provide awareness to senior managers and provide an opportunity to trend the condition. The inspectors concluded this issue was a performance deficiency of minor significance based on the actions taken by Entergy staff at that time which included chemistry results that supported Entergys assessment the water was not indicative of CST water chemistry and tritium levels were well below regulatory limits for release to the environment.
 
===.6 Semi-Annual Trend Review===
{{IP sample|IP=IP 71152|count=1}}
 
====a. Inspection Scope====
In July 2009, inspectors reviewed Entergy staffs progress in implementing corrective actions identified in 2008 to address Human Performance issues as outlined in Entergys Human Performance Improvement Plan with a focus on specific efforts since January 2009. The inspectors evaluated staff performance improvement plans and actions using inspection guidance in Inspection Procedure 71152, Identification and Resolution of Problems.
 
Specifically, the inspectors assessed Entergys progress in addressing human performance by evaluating whether Entergys internal milestones were being monitored and consistently met and whether adjustments in approach were made when necessary. This inspection focused on the actions implemented since January 2009.
 
The inspectors conducted a review of the applicable condition reports (CRs), corrective action assignments (CAs), focused self-assessments, Quality Assurance group assessments, and causal evaluations for human performance events and errors. The inspectors also reviewed Entergy internal performance indicators related to their performance improvement plan, and reviewed a sample of revised procedures in order to assess the adequacy of the performance plan and effectiveness of corrective actions.
 
====b. Findings and Observations====
No findings of significance were identified.
 
In late December 2008, NRC inspectors independently reviewed the causal evaluation and corrective actions focused on an emerging trend, identified by Entergy, and associated with human performance errors. Entergy staff and managers identified several events, attributable to human performance errors that occurred at Indian Point (both units) in 2008, which resulted in personal injury and/or equipment failures. The inspectors determined that Entergy managers recognized this adverse trend in human performance, and developed a Human Performance Program to address the causes of the events, and to assist in the prevention or mitigation of future occurrences. The inspectors noted that the Human Performance Program included actions to understand the causes of human performance errors, to reduce these human performance errors in the future, and to monitor future performance.
 
The inspectors determined Entergy staff and managers developed station-wide communication tools, training plans, and adjusted the site business plan to address these common causes of human performance errors. New communication tools developed included Safety and Human Performance Stand Downs and periodic human performance bulletins. The Safety and Human Performance Stand Downs were used to develop a forum to reinforce site human performance expectations and discuss recent human performance error events. Entergy managers also scheduled future stand downs to coincide with major evolutions on site in 2009, such as the Unit 3 refueling outage.
 
The inspectors noted that Entergy staff developed a Human Performance Simulator and Work Management Academy to provide training on human performance traps, human performance tools, and to improve work planning and execution. The Human Performance Simulator focuses on reinforcing the proper threshold for identifying error traps and the effective use human performance tools to accomplish tasks. Operations and maintenance departments have completed this training, and it will now be included as annual refresher training for their department personnel. The Work Management Academy was required for all supervisory personnel and reinforced Entergys work management model and procedures. Entergy staff and managers also developed its Thought Improvement Process (TIP) Initiative to encourage employees to provide constructive feedback to improve the sites human performance.
 
The inspectors also noted that Entergy staff and managers established commitments to monitor future human performance at Indian Point. In particular, human performance indicators and self-assessment results would be used to monitor the effectiveness of the current programs and for evaluation of future trends in human performance. The inspectors concluded that Entergy took action to address the sites emerging adverse human performance trend. The programs established within Entergys Human Performance program were determined to be reasonable to address the recent human performance.
 
During the July 2009 semi-annual trend review, inspectors determined that Entergy staff continued to make progress in implementing their corrective action plans to address human performance issues related to error prevention and to make adjustments to those actions based on the results of self-assessments, performance indicators, and benchmarking. For example, based on observations of supplemental workers during the recent Unit 3 refueling outage, actions were being developed to provide additional oversight of supplemental workers. The inspectors also noted that, in accordance with previous corrective actions, Entergy staff and managers had:
* Continued to use the Human Performance Simulator to train various departments, and to check and adjust development of dynamic learning activities in the simulator;
* Implemented a standard schedule for site wide stand downs during outage and non-outage periods;
* Revised pre-job briefing procedures to include signature accountability,
* Implemented a task/job observation program aligned with the work control process and Most Error Likely Task-focused crew assessments;
* Assigned experienced mechanics, technicians, and operators to procedure groups;
* Reinforced critical procedure steps through the use of special markings, briefs, and feedback;
* Filled key personnel vacancies previously identified as necessary to strengthen the organizations effectiveness in preventing human error;
* Improved adherence to online and outage work management milestones;
* Improved effectiveness of work package walk downs and feedback;
* Established weekly work package quality meetings.
 
Additionally, the inspectors noted that Entergy has developed additional performance indicators to assist in monitoring progress in addressing human errors, and is planning to conduct annual Human Performance training to first-line supervisors and above.
 
The recent trend in human performance related to error prevention indicated that corrective actions, to date, have not resulted in a decrease in the human error rate trend, primarily due to issues that occurred during the Unit 3 refueling outage. Notwithstanding, the inspectors concluded that station management has adjusted its actions/focus as a result of its evaluation of additional performance information, especially from the outage. The programs and actions established within Entergys Human Performance program were determined to be reasonable to address the recent human performance issues related to error prevention.


{{a|4OA3}}
{{a|4OA3}}
==4OA3 Event Follow-up .................................................................................................... 21==
 
==4OA3 Event Follow-Up==
{{IP sample|IP=IP 71153|count=2}}
 
===.1 Reactor Trip on April 3, 2009, Due to Low Steam Generator Water Levels===
====a. Inspection Scope====
The inspectors responded to the control room on April 3, 2009, following a manual insertion of all control rods (manual reactor trip) by control room operators due to lowering water levels in all four steam generators (SGs) due to a combination of an unexpected 21 main boiler feed pump (MBFP) shutdown and failure of the main turbine generator to runback after the loss of the 21 MBFP. The main turbine has a non-safety related control circuit that automatically reduces the load on the turbine to a predefined level if the circuit senses plant power is greater than 85% and a MBFP is rotating at a rate of less than 3300 revolutions per minute (rpm). The purpose of this control circuit is to reduce the potential for a reactor trip due to a loss of a single MBFP. Because this circuit did not function, only the 22 MBFP, which is rated for about 60% power, was supplying feed water to the SGs. At the time, the SGs were producing 100% steam flow because the turbine runback circuitry did not function to runback and resulted in water levels decreasing in the four SGs. Control room operators inserted a manual reactor trip based on their conclusion they could not restore sufficient feed water to the SGs, or reduce the steam demand from the turbine, prior to an automatic reactor trip on low water level in the SGs.
 
Entergy personnel investigated the unexpected loss of the 21 MBFP and identified a stainless steel tube leak in the high pressure oil system associated with the 21 MBFP control system that caused reduced oil pressure below the MBFPs low oil pressure turbine trip setpoint. Entergy personnel determined the tube failed due to vibration induced metal fatigue. Entergy personnel performed extent of condition inspections on similar components in the 21 and 22 MBFP control oil systems. Entergy replaced the damaged tube and restored the system to service.
 
Entergy engineers and maintenance technicians initiated troubleshooting activities on the main turbine runback circuitry to determine the cause of the turbine runback failure during the transient. Entergy personnel were not able to identify a malfunctioning component in the runback circuitry. Entergy technicians tested the inputs to the system and tested the circuits operation including the MBFP turbine tachometer dropout relays and did not identify the malfunction experienced with the turbine runback circuitry. Station management implemented its decision making process and determined it was safe to startup the plant based on completed troubleshooting activities of this non safety-related circuitry in which operators are trained to respond to this scenario.
 
The inspectors performed system walkdowns, interviewed personnel, and reviewed design basis documents, troubleshooting plans, station procedures, and engineering evaluations.
 
====b. Findings====
The inspectors concluded that operators responded appropriately to the transient in accordance with their procedures and training. The inspectors also concluded that Entergys efforts at identifying the cause and extent of condition was adequate. Furthermore, the inspectors concluded that Entergys troubleshooting efforts to identify potential problems with the turbine runback circuitry were reasonable to demonstrate this function prior to plant restart. The following self-revealing finding was identified in relation to the installation of the MBFP hydraulic control system:
 
=====Introduction.=====
A self-revealing Green finding was identified because Entergy personnel did not establish adequate instructions in a design change package which resulted in incorrectly installed tubing in the 21 main boiler feed water pump (MBFP) hydraulic control system that subsequently failed due to fatigue.
 
=====Description.=====
On April 3, 2009, the 21 MBFP tripped off-line and steam generator water levels began to lower. The automatic main turbine runback circuitry did not actuate as designed to reduce main turbine steam demand. The control room operators attempted to manually reduce the main turbine steam demand but steam generator water inventory reduced to a level that required the operators to manually trip the reactor. Entergy personnel investigated the 21 MBFP trip and identified that a broken tube fitting resulted in high pressure control oil leaking to the oil sump and a subsequent trip of the 21 MBFP on low oil pressure.
 
Entergy staff sent the failed fitting to a vendor to be analyzed. The analysis determined the tubing likely failed from chronic cyclical stresses. Entergy personnel determined the tubing was installed incorrectly in 1986 when an engineering modification was implemented to upgrade the MBFP control system. Specifically, the stainless steel tubing was installed in a straight line with inadequate room to flex or expand, contrary to vendor installation instructions and existing maintenance procedures for installing tubing and Swagelok fittings.
 
The vendor and maintenance procedures required that tubing be installed with U shape bends to allow for expansion and flexing. Entergys root cause identified the engineering modification package used at the time of installation did not provide guidance on the tubing layout and did not provide specific instructions for tubing installation that were available in vendor manuals and site maintenance procedures. The root cause team confirmed that Swagelok installation manuals dating back to 1972 contained information on the proper use of gap gauges and examples of correct/incorrect tubing routing installations. The stations design change procedure required (section 5.3.11, Detailed Design Activities) that the design change package included specific installation and inspection requirements that are not addressed in existing installation specifications including known precautions and limitations.
 
Contrary to the design change procedure, specific instructions were not provided to ensure Swagelok fittings and tubing runs were installed in accordance with station procedures or vendor requirements including precautions to never run tubing in a straight run between rigid mounts. The inspectors determined it was reasonable for the station to provide correct guidance to the field installers in 1986 because the design change process required specific instructions to be provided and the design change packages were reviewed by multi-disciplined teams, including the maintenance department, who were cognizant of the standards for the installation of Swagelok fittings.
 
Entergy personnel inspected the MBFP control system tubing for the 21 and 22 MBFPs on Unit 2 and the 31 and 32 MBFPs on Unit 3. Entergy personnel identified a similar configuration on the 22 MBFP and replaced the tubing with the proper arrangement; the tubing on the Unit 3 MBFPs was found to be installed properly. Entergy personnel also developed corrective actions to evaluate training improvements for the installation or maintenance of tubing and compression fittings for site and supplemental personnel.
 
Entergy personnel plan to inspect and evaluate other compression fitting installations associated with other high speed rotating equipment.
 
=====Analysis.=====
The inspectors determined that a performance deficiency existed in that Entergy engineers did not provide adequate instructions to workers in order to install tubing in the MBFP control system in accordance with their design change program and vendor specifications.
 
The finding was more than minor because it was associated with the design control attribute of the Initiating Events cornerstone and affects its objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the incorrectly installed MBFP control tubing resulted in a loss of the 21 MBFP and, ultimately, a reactor trip due to low steam generator water level. In accordance with IMC 0609, Attachment 0609.04, Initial Screening and Characterization of Findings, the inspectors conducted a Phase 1 screening and determined this finding required a Phase 2 analysis because the finding contributed to both the likelihood of a reactor trip and the likelihood that the mitigation equipment functions will not be available (loss of redundancy in the feedwater system for other initiating events).
 
The inspectors determined the finding was of very low safety significance (Green) using the Phase 2 Indian Point Unit 2 Risk-Informed Inspection Notebook, in accordance with IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations. The inspectors determined that the exposure time was <3 days because the failure mechanism was a slow cyclic fatigue that resulted in failure only after the material had degraded to an unacceptable thickness and had demonstrated acceptable operation over the previous year while the MBFP was in operation. Using the <3 day exposure time, the inspectors solved: the Transient with Loss of Power Conversion System (TPCS) worksheet, increasing the likelihood of the initiating event by one order of magnitude, to address the increased likelihood of a reactor trip; and the Transients with Power Conversion System Available (TRANS) and Loss of Component Cooling Water (LOCCW) worksheets to address the loss of feedwater pump redundancy. This Phase 2 SDP estimated the increase in core damage frequency to be in the range of 1 in 50,000,000 years of reactor operation (low E-8 range). This range represents a finding of very low safety significance (Green). The dominant core damage sequence was a TPCS initiating event mitigated by the remaining ability to remove heat from the reactor core using auxiliary feed water or the primary bleed and feed functions.
 
The inspectors determined there was no cross-cutting aspect associated with the finding because the performance deficiency did not reflect current licensee performance.
 
Specifically, the performance deficiency occurred over 20 years ago and procedures have been improved in the design control, work control and vendor control processes since 1986 that reduce the likelihood of vendors working on equipment without the sufficient training or work instructions.
 
=====Enforcement.=====
Enforcement action does not apply because the performance deficiency did not involve a violation of a regulatory requirement, and the equipment involved is not safety related. Because this finding does not involve a violation of regulatory requirements and has very low safety significance, it is identified as FIN 05000247/2009003-01, Inadequate Design Change Package for Installation of Main Boiler Feed Pump Control System Tubing.
 
===.2 (Closed) LER 2009-001-00, Technical Specification Prohibited Condition Due to a===
Surveillance Requirement Not Previously Performed for the Atmospheric Steam Dump Valve Local Nitrogen Controls.
 
The inspectors reviewed Licensee Event Report (LER) 2009-001-00 dated April 27, 2009, to verify the LER was completed in accordance with 10 CFR 50.73 and that corrective actions identified were appropriate. The inspectors reviewed the circumstances of the January 2009 event and entries into the corrective action program including the apparent cause analysis.
 
The LER reported that a TS-required surveillance requirement (SR 3.3.4.2) was not previously performed for the nitrogen back-up supply to the steam generator atmospheric dump valves (ADVs). Specifically, Entergy personnel did not verify the nitrogen backup supply control circuit and transfer switch to the steam generator ADVs were capable of performing their intended function. Entergy personnel discovered this following testing of an engineering modification that installed an additional nitrogen supply for the atmospheric steam dump valves (ADVs) and determined that two of the four ADVs positioners were setup incorrectly. The equipment errors resulted in the failure of the valves to stroke open using the nitrogen backup supply; however, because of the design of the system, Entergy personnel determined the valves were able to stroke open using the normal station air supply. Because all four valves could operate using the station air system, and at least one ADV was operable using the nitrogen backup supply at all times in accordance with design requirements, the inspectors determined that no complete loss of ADV function had occurred. Entergy personnel repaired the positioners and established corrective actions to develop tests for the nitrogen backup supply and verified that the TS surveillance requirements have tests associated with them and are properly scheduled. Entergy documented the issues described above in CRs: IP2-2009-00062, -00069, -00077, -00137, and -00983.
 
The LER described a violation of TS 3.3.4, Remote Shutdown. The enforcement aspects of this finding are discussed in Section 4OA7. This LER is closed.


{{a|4OA5}}
{{a|4OA5}}
==4OA5 Other Activities ...................................................................................................... 27==


{{a|4OA6}}
==4OA5 Other Activities==
==4OA6 Meetings, including Exit ......................................................................................... 27==
Quarterly Resident Inspector Observations of Security Personnel and Activities
ATTACHMENT:
 
====a. Inspection Scope====
During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that these activities were consistent with Entergy security procedures and applicable regulatory requirements. Although these observations did not constitute additional inspection samples, the inspections were considered an integral part of the normal, resident inspector plant status reviews during implementation of the baseline inspection program.
 
====b. Findings====
No findings of significance were identified.
 
{{a|4OA6}}
 
==4OA6 Meetings==
===Exit Meeting Summary===
On July 22, 2009, the inspectors presented the inspection results to Mr. Joseph Pollock and other Entergy managers and staff, who acknowledged the inspection results. Entergy staff identified documents which were to be considered proprietary and handled as such.
 
{{a|4OA7}}
 
==4OA7 Licensee-Identified Violations==
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy, for being dispositioned as a Non-Cited Violation.
* Technical Specification Surveillance Requirement Not Previously Performed for Steam Generator Atmospheric Dump Valves
 
As described above in Section 4OA5.2, on January 7, 2009, following installation and post-work testing of an additional backup nitrogen supply to the ADVs, Entergy personnel identified that surveillance tests for the nitrogen backup supplies to the ADVs were never performed contrary to TS surveillance requirement 3.3.4.2.
 
The inspectors determined this constituted a violation of TS 3.3.4, Remote Shutdown, which includes the TS surveillance requirement to verify that the nitrogen backup supply control circuit and transfer switch to the steam generator ADVs are capable of performing their intended function. Contrary to this requirement, Entergy personnel did not verify the functionality of the control circuitry associated with the nitrogen backup supply to the ADVs.
 
The inspectors determined this issue was of very low safety significance (Green) per SDP Phase 1 screening because the safety function of the ADVs was not lost. Specifically, the inspectors determined the remote shutdown function for the steam generator requires only one ADV to be operable. All four ADVs were capable of being operated with the normal station air supply. Entergy personnel entered the issues into the corrective action program as CR-IP2-2009-00062, -00069, -00077, -00137, and -00983.
 
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
.......................................................................................... A-1   
Entergy Personnel
==LIST OF ITEMS==
: [[contact::J. Pollock]], Site Vice President
OPENED, CLOSED AND DISCUSSED ................................................ A-2   
: [[contact::A. Vitale]], General Manager, Plant Operations
==LIST OF DOCUMENTS REVIEWED==
: [[contact::K. Davison]], Assistant General Manager, Plant Operations
............................................................................... A-2
: [[contact::P. Conroy]], Director of Nuclear Safety Assurance
==LIST OF ACRONYMS==
: [[contact::B. Sullivan]], Emergency Planning Manager
..................................................................................................... A-7
: [[contact::A. Williams]], Site Operations Manager
Enclosure
: [[contact::S. Verrochi]], System Engineering Manager
: [[SUMMAR]] [[Y]]
: [[contact::T. Orlando]], Director, Engineering
: [[OF]] [[]]
: [[contact::R. Walpole]], Licensing Manager
: [[FINDIN]] [[]]
: [[contact::T. Cole]], Project Manager
GS  IR 05000286/2009-003; 04/01/2009 - 06/30/2009; Indian Point Nuclear Generating Unit 3; Event Follow-up.
 
This report covered a three-month period of inspection by resident and region-based inspectors. Two findings of very low significance (Green) were identified, one of which was also determined to be a non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
Determination Process."  The cross-cutting aspect for each finding was determined using
===Opened and Closed===
: [[IMC]] [[0305, "Operating Reactor Assessment Program."  Findings for which the significance determination process (]]
: 05000247/2009003-01 FIN
: [[SDP]] [[) does not apply may be Green, or be assigned a severity level after]]
 
: [[NRC]] [[management review. The]]
Inadequate Design Change Package
: [[NRC]] [['s program for overseeing safe operation of commercial nuclear power reactors is described in]]
 
: [[NUR]] [[]]
for Installation of Main Boiler Feed
: [[EG]] [[-1649, "Reactor Oversight Process," Rev. 4, dated December 2006.]]
 
: [[A.]] [[]]
Pump Control System Tubing
NRC-Identified and Self-Revealing Findings  Cornerstone: Initiating Events  * Green. The inspectors identified a non-cited violation (NCV) of 10 CFR 50.65(a)(4), because Entergy personnel did not adequately assess and manage increased risk associated with planned corrective maintenance. Specifically,
 
Entergy staff did not include in their maintenance risk assessment the increase in shutdown plant risk for the repacking of
(Section 4OA3)  
: [[SP]] [[-954A, a non-isolable root isolation from the reactor coolant system associated with the sampling system, during fuel reload operations. The inadequate risk assessment and management of the risk associated with this job resulted in a short duration leak in the]]
RCS. The inspectors determined this finding affected the Initiating Event cornerstone and was more than minor because the risk assessment did not consider maintenance activities that could increase the likelihood of initiating events. The inspectors determined this finding was of very low safety significance because
Entergy staff maintained required mitigation capability in accordance with IMC 0609, Appendix G, Attachment 1, Checklist 4. The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance because personnel did not appropriately plan work activities by incorporating appropriate risk insights, job site conditions, contingencies, and abort criteria
consistent with nuclear safety. (H.3(a)) (Section
: [[4OA]] [[3)  * Green. A self-revealing finding of very low safety significance was identified because Entergy personnel did not have adequate procedures appropriate for maintenance associated with air-operated valves. Specifically, existing Entergy maintenance procedures did not ensure that the 33 steam generator (]]
SG) feedwater regulating valve (FRV) positioner feedback arm connecting linkage hardware was properly secured following maintenance. As a result, on May 15, 2009, this linkage became disconnected which led to SG level oscillations that
required a manual reactor trip by control room operators. Entergy personnel repaired the valve positioner feedback arm connecting linkage, identified the
Enclosure main cause during a post-transient review, performed extent of condition inspections on similar valves susceptible to the same linkage deficiency, and completed a root cause analysis within the corrective action program under condition report (CR)-IP3-2009-02368. The inspectors determined the finding is more than minor because the finding is associated with the equipment performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during
shutdown as well as power operations. Specifically, the inadequate procedures resulted in the failure of a non-safety-related portion of the
: [[33 SG]] [[]]
: [[FRV]] [[and resulted in a manual reactor trip. The inspectors evaluated the significance of the finding using]]
: [[IMC]] [[0609, Attachment 4, and determined this finding did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would be unavailable. Consequently, the finding is of very low safety significance (Green). The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance because Entergy staff did not ensure that complete, accurate and up-to-date procedures were available to perform appropriate maintenance on air-operated valve positioners associated with the 33]]
SG FRV. 
(H.2(c))  B. Licensee-Identified Violations  None.
Enclosure
: [[REPORT]] [[]]
DETAILS  Summary of Plant Status
Indian Point Unit 3 began the inspection period in a shutdown condition for continuation of refueling outage No. 15 (3R15). The unit achieved initial criticality on April 15, 2009, and reached full power on April 19. Operators manually tripped the Unit 3 reactor May 15 due to a degraded feedwater regulating valve. Operators restored the plant to full power on May 16. Subsequently, problems associated with main boiler feedwater pumps (MBFP) resulted in a
downpower to 75% on May 28 and an automatic reactor trip due to steam generator water level control issues. Following repairs to the
: [[31 MBFP]] [[, the unit was re-started on May 29 and was stabilized at 55% power to perform repairs to the 32]]
: [[MBFP.]] [[Continuing problems with the]]
: [[MBFP]] [[control systems resulted in a subsequent shutdown on May 31 to perform repairs. Subsequently, on June 5, operators returned the plant to 65% power while maintenance staff repaired the 32]]
: [[MBFP.]] [[On June 23, the]]
: [[32 MB]] [[]]
FP was returned to service and operators restored reactor power to 100%. Unit 3 remained at full power for the remainder of the
inspection period. 1.
: [[REACTO]] [[R]]
SAFETY  Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01 - 3 samples)  .1 Hot Weather Preparations
a. Inspection Scope  Using procedure
: [[OAP]] [[-048, "Seasonal Weather Preparation," Rev. 4, and the Updated Final Safety Analysis Report (]]
UFSAR) as a reference, the inspectors reviewed preparations for hot weather and performed walkdowns of plant areas during the week of
June 15, 2009. As part of the walkdown, local area temperatures were checked, as well as the operability of ventilation and air conditioning systems to ensure that the plant was prepared for warm weather conditions. The inspectors focused on the auxiliary boiler feed pump room, control room, and the emergency diesel generator room ventilation systems.
b. Findings  No findings of significance were identified.  .2 Summer Readiness of Offsite and Alternate AC Power Systems
a. Inspection Scope  The inspectors performed a detailed review of the offsite and alternate AC power system readiness, and performed a walkdown to observe the material condition of the Buchanan switchyard and on-site switchyard areas and components. This review also included an
assessment of Entergy operator's response to 345 kV grid disturbances that occurred on
Enclosure April 24th, April 30th, May 7th, June 9th and June 15th, to verify appropriate interface and protocols exist between Entergy staff and the offsite power transmission system operators, such as process, policies and procedures. The inspectors reviewed completed and outstanding work orders for these power systems and components,
assessed the adequacy of corrective actions for identified, degraded conditions, and observed the performance of a monthly, on-site switchyard inspection activity conducted on June 17, 2009. The documents reviewed during this inspection are listed in the Attachment.
b. Findings  No findings of significance were identified.  .3 External Flooding Assessment of Manhole No. 34    a. Inspection Scope  The inspectors evaluated Entergy personnel's actions to mitigate the effects of periodic groundwater coverage of safety-related and augmented quality-related cables located in Manhole 34, as well as the effects of groundwater and rain water that collects in the manhole over time. This review verified whether Entergy had appropriate water
mitigation strategies, cable inspection and testing, and cable support inspections, to ensure continued operability and functionality of the associated components that are supplied electrical power by the cables that route through this manhole. In particular, the inspectors reviewed Entergy staff's actions to correct a degraded condition that occurred in 2006, which involved a non-functional support for backup service water (SW) pump
No. 38, as detailed in condition report
: [[CR]] [[-]]
IP3-2006-01662. The inspectors also reviewed Entergy engineers' assessments that concluded the support did not provide a safety function. Additionally, the inspectors entered Manhole 34 to inspect and observe the material condition of the cables and associated cable supports. Documents reviewed during this inspection are located in the Attachment. b. Findings  No findings of significance were identified.
1R04 Equipment Alignment  .1 Partial System Walkdowns (71111.04Q - 3 samples)    a. Inspection Scope  The inspectors performed partial system walkdowns to inspect Entergy operators'
performance in maintaining the proper equipment alignment of redundant or diverse trains and components during periods of system train unavailability, and where applicable, following return to service after maintenance. The inspectors reviewed system procedures, the Updated Final Safety Analysis Report (UFSAR), and system drawings to verify that the alignment of the applicable system or component supported
its required safety functions. The inspectors also reviewed applicable condition reports
Enclosure or work orders to ensure that Entergy personnel had identified and properly addressed equipment deficiencies that could potentially impair the capability of the available train. The documents reviewed during this inspection are listed in the Attachment.
The inspectors performed partial walkdowns of the following systems or components, which represented three inspection samples:  * 31 and 32 emergency diesel generators (EDGs) electrical alignment while the
: [[33 EDG]] [[was out-of-service for maintenance on May 18, 2009; * 32 and 33]]
: [[EDG]] [[s while the]]
: [[31 EDG]] [[was out-of-service for 2-year and 4-year planned maintenance activities, and exhaust muffler replacement on June 16-17, 2009; and  * 31]]
EDG return-to-service following replacement of a failed pre-lube pump on June 17, 2009.
b. Findings  No findings of significance were identified.  .2 Complete System Walkdown (71111.04S - 1 sample)    a. Inspection Scope  The inspectors performed a complete system walkdown of accessible portions of the auxiliary feedwater (AFW) system to identify discrepancies between the existing equipment alignment and the required alignment for the current plant conditions. The inspectors reviewed operating procedures, surveillance tests, equipment lineup check-
off lists, and the
: [[UFSAR]] [[, to determine if the]]
: [[AFW]] [[system was aligned to perform its required safety functions. The inspectors reviewed a sample of condition reports that were written to address deficiencies associated with the]]
: [[AFW]] [[system, and verified that these deficiencies were appropriately evaluated and/or resolved. The documents reviewed during this inspection are listed in the Attachment. The walkdown of the]]
AFW
system represented one inspection sample. b. Findings  No findings of significance were identified. 1R05 Fire Protection  .1 Annual Fire Drill (71111.05A - 1 sample)
a. Inspection Scope  On June 10, 2009, the inspectors observed an unannounced fire brigade drill that utilized on-watch fire brigade members from the shift operations crew. The drill was conducted in accordance with Entergy's preplanned drill scenario that involved a simulated electrical fire with associated hazards in the vicinity of electrical distribution switchgear panel MCC 36A, which is located in the plant auxiliary building, a
Enclosure radiologically-controlled area. The inspectors evaluated the performance of the fire brigade during the drill, consistent with the pre-planned drill scenario, to verify the following attributes: * The fire brigade members properly donned protective clothing/turnout gear, which included simulated use of self-contained breather apparatus (SCBA) equipment; * Fire hose lines were capable of reaching the fire hazard locations, were laid out without flow restrictions, and were simulated being charged with water; * Brigade members entered the fire area in a controlled manner, and utilized appropriate equipment consistent with they type of fire simulated during the drill; * Sufficient fire-fighting equipment was brought to the scene by the fire brigade; * The fire brigade leader's directions during implementation of the pre-fire plans for the designated fire area were thorough, clear and effective; * Radio communications, as well as face-to-face communications with the plant operators and fire brigade members were efficient and effective; * Control room personnel followed applicable procedures for response to a fire and identified the appropriate Emergency Action Levels and associated notifications consistent with implementing procedures and site Emergency Plan; * The drill report contained appropriate post-drill critique comments and identified deficiencies consistent with the objectives and acceptance criteria of the drill; and; * Appropriate deficiencies were entered into the corrective action program;  Documents reviewed during this inspection are listed in the Attachment. b. Findings  No findings of significance were identified.  .2 Quarterly Fire Area Walkdowns (71111.05Q - 6 samples)
a. Inspection Scope  The inspectors conducted tours of the Unit 3 vapor containment (VC) fire areas to assess the material condition and operational status of applicable fire protection features. The inspectors verified, consistent with the applicable administrative procedures, that: combustible material and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with Entergy's fire protection program. Additionally, the inspectors verified that outage-related activities conducted inside the
: [[VC]] [[, which resulted in the placement of numerous, additional equipment and support material throughout the]]
VC, would not
impact the adequate implementation of fire protection measures. The inspectors also evaluated the fire protection program against the requirements of License Condition 2.K. The documents reviewed during this inspection are listed in the Attachment.
Enclosure This inspection represented six inspection samples and was conducted in the areas covered by the following Pre-Fire Plans:  * Pre-Fire Plan No. 301; * Pre-Fire Plan No. 302; and * Pre-Fire Plan No. 303. b. Findings  No findings of significance were identified. 1R11 Licensed Operator Requalification Program (71111.11Q - 1 sample)  Quarterly Resident Inspector Evaluation
a. Inspection Scope  On June 22, 2009, the inspectors observed licensed operator simulator training to verify that operator performance was adequate, and the evaluators were identifying and documenting crew performance problems. The inspectors evaluated the performance of risk significant operator actions, including the use of emergency operation procedures. The inspectors assessed the clarity and the effectiveness of communications, the
implementation of appropriate actions in response to alarms, the performance of timely control board operation and manipulation, and the oversight and direction provided by the control room supervisor. The inspectors reviewed simulator fidelity to verify correlation with the actual plant control room, and to verify that differences in fidelity that could potentially impact training effectiveness were either identified or appropriately
dispositioned. Licensed-operator training was evaluated against the requirements of 10 CFR Part 55, "Operator Licenses."  The documents reviewed during this inspection are listed in the Attachment. This observation of operator simulator training represented one inspection sample.
b. Findings  No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12 - 2 samples)    a. Inspection Scope  The inspectors reviewed performance-based problems that involved selected structures, systems, and components (SSCs), to assess the effectiveness of maintenance activities
and to verify activities were conducted in accordance with site procedures and 10 CFR 50.65 (The Maintenance Rule). The reviews focused on: * Evaluation of Maintenance Rule scoping and performance criteria; * Verification that reliability issues were appropriately characterized; * Verification of proper system and/or component unavailability;
Enclosure * Verification that Maintenance Rule (a)(1) and (a)(2) classifications were appropriate; * Verification that system performance parameters were appropriately trended; and * For SSCs classified as Maintenance Rule (a)(1), that goals and associated corrective actions were adequate and appropriate for the circumstances. The inspectors also reviewed system health reports, maintenance backlogs, and Maintenance Rule basis documents. The documents reviewed during this inspection are listed in the Attachment. The following Unit 3 systems and/or components were reviewed and represented three inspection samples:
* 31 and 32 Main Boiler Feed Pump deficiencies (3R15 to present); and * Emergency diesel generators service water temperature control valve stroke time failures (CR IP3-2009-02132);    b. Findings  No findings of significance were identified.
1R13 Maintenance Risk Assessments/Emergent Work Control (71111.13 - 5 samples)    a. Inspection Scope  The inspectors reviewed maintenance activities to verify that the appropriate on-line and
shutdown risk assessments were performed prior to removing equipment for work as required by
: [[10 CFR]] [[50.65 (a)(4). When planned work scope or schedules were altered to address emergent or unplanned conditions, the inspectors verified that the plant risk was promptly reassessed and managed. Additionally, the inspectors utilized]]
IMC 0609, Appendix G, during various refueling outage periods, to assist in the evaluation of Entergy's shutdown risk assessments. The documents reviewed during this inspection are listed in the Attachment. The following activities represented five inspection
samples:  * Transition to/from shutdown and online risk assessments that occurred on April 12-13, 2009; * Planned risk for various maintenance activities, including the No. 32 boric acid transfer pump, conducted on May 14, 2009; * Planned risk during No. 33 emergency diesel generator and Appendix R diesel activities on May 17 to 18, 2009; * Emergent risk following a fault that occurred on the 138kV cross-connect line between Unit 2 and Unit 3 on May 18, 2009; and * Planned risk during 138kV crosstie outage and No. 33 EDG maintenance activities on May 18, 2009. b. Findings  No findings of significance were identified.
Enclosure 1R15 Operability Evaluations (71111.15 - 4 samples)    a. Inspection Scope  The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications. These reviews included verification that operability determinations were performed in accordance with procedure
: [[ENN]] [[-]]
OP-104, "Operability Determinations."  The inspectors assessed the technical adequacy of the
evaluations to ensure consistency with the
: [[UFSAR]] [[and associated design and licensing basis documents. The documents reviewed are listed in the Attachment. The following operability evaluations were reviewed and represented four inspection samples:  *]]
: [[CR]] [[-IP3-2009-01200: 32 emergency diesel generator power factor acceptability during 3-PT-R160B, "Capacity Test." *]]
: [[CR]] [[-]]
: [[IP]] [[3-2009-02004:  31A Manhole non-functional cable support and seismic criteria evaluation; *]]
: [[CR]] [[-]]
: [[IP]] [[3-2009-01829:  32 Atmospheric Steam Dump drifted fully open while controller in manual; and *]]
: [[CR]] [[-]]
IP3-2009-01245:  Bearing degradation identified during maintenance on the 32 AFW pump.
b. Findings  No findings of significance were identified. 1R18 Plant Modifications (71111.18 - 2 samples)  .1 Setpoint Change of Safety Injection Pump Discharge Relief Valve (SI-855)   a. Inspection Scope  The inspectors reviewed the design documentation associated with the increase in the relief setpoint on SI-855, from 1575 psig to 1670 psig. The inspectors reviewed plant
design documents and calculations to ensure the increase in setpoint would not adversely impact normal and off-normal plant operations. Specifically, the inspectors verified that the increase in allowed pressure would not adversely affect the Safety Injection pumps and piping during normal plant operations with design allowed check valve leakage as well as emergency operating scenarios. Pre-installation testing of the
new relief valve was reviewed along with the post-installation testing. b. Findings  No findings of significance were identified.


Enclosure .2 Core Exit Thermocouple H05 Substitution with K03    a. Inspection Scope  The inspectors reviewed the design documentation associated with the substitution of Train "A" degraded core exit thermocouple (CET) H05, with Train "B"
===Closed===
: [[CET]] [[K03. This substitution of]]
: 05000247/2009001-00
: [[CET]] [[s located in Quadrant]]
: [[II]] [[of the reactor vessel, essentially removed]]
CET H05 from service, and utilized its existing wiring to ensure CET K03 would be viewable from the safety parameter displays in the control room. The inspectors verified
the adequacy of the modification to ensure consistency with the design and licensing bases, including the
: [[TS]] [[,]]
UFSAR, and associated calculations, procedures, and drawings. This verification included a review of attributes, such as engineering design change program requirements, and proposed procedure changes that ensured CET K03 would be identified as H05 on the applicable control room panel displays. During implementation of the modification, the inspectors verified that appropriate
configuration and testing controls were utilized, which ensured appropriate interface existed between the various activities to ensure continuity of safe plant operations. Following implementation, the inspectors verified that post-modification testing criteria were adequate and that acceptable results were obtained. Additionally, the inspectors
verified that applicable operating and maintenance procedures were appropriately revised consistent with the requirements of the modification. b. Findings  No findings of significance were identified. 1R19 Post-Maintenance Testing (71111.19 - 5 samples)    a. Inspection Scope  The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems, and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and plant personnel. The inspectors verified that: test acceptance criteria were clear; tests
demonstrated operational readiness and were consistent with design basis documentation; test instrumentation had current calibrations and appropriate range and accuracy for the application; tests were performed as written; and applicable test prerequisites were satisfied. Upon completion of the tests, the inspectors verified that equipment was returned to the proper alignment necessary to perform its safety function. Post-maintenance testing was evaluated against the requirements of
: [[10 CFR]] [[50, Appendix B, Criterion]]
XI, "Test Control."  The following post-maintenance activities were
reviewed and represented seven inspection samples:  * Repair
: [[32 EDG]] [[fuel oil day tank level control valve,]]
DF-LCV-1208A; * Replace rotating assembly for the 32 boric acid transfer pump; * 34 reactor coolant pump (RCP) seal injection containment isolation valve (CH-MOV-250D) maintenance activities;
Enclosure * Replacement of
: [[32 AFW]] [[pump cutback controller; and * Replacement of positioner feedback arm connecting linkage on the 33]]
: [[SG]] [[]]
: [[FRV.]] [[b. Findings  No findings of significance were identified. 1R20 Refueling and Outage Activities (71111.20)  .1 Refueling Outage No. 15 (partial for outage credited and started in 1st quarter 2009)    a. Inspection Scope  The inspectors observed and/or evaluated the selected outage activities listed below to verify that (1) shutdown risk was considered during schedule preparation and implementation, and high risk significant evolutions such as mid-loop or reduced inventory conditions; (2) defense-in-depth (]]
DID) measures were utilized to mitigate impacts on key safety functions (e.g., reactivity control, electrical power availability, containment integrity, etc.) due to plant configuration control changes and ensure compliance with technical specifications and the operating license throughout the outage
period; and (3) risk significant activities were conducted in accordance with procedures and evaluated in a manner appropriate for the circumstances.  * Fuel transfer from the spent fuel pool into the vapor containment, and final core reload activities; Special nuclear material (SNM) accountability, transfer and control; * Plant/reactor startup and shutdown, and heatup/cooldown activities (in accordance with
: [[TS]] [[limits); * Changes in daily plant risk and implementation of]]
: [[DID]] [[measures; * Verified mini-containment integrity and]]
: [[RHR]] [[valve maintenance; * Post-outage boric acid inspection inside the vapor containment to assess effectiveness of unidentified leakage monitoring and compliance with]]
TS, as well as effectiveness of boric acid cleanup of issues identified post-shutdown; * Open outage constraints (work orders and condition reports) were reviewed to verify appropriate disposition of issues, both technical and/or administratively, to
ensure compliance with procedural and/or
: [[TS]] [[requirements; * Performed a final vapor containment closeout inspection to ensure debris and equipment were appropriately removed or restrained to mitigate potential impact on reactor and containment sumps; verified compliance with]]
: [[OAP]] [[-007, "Containment Entry and Egress," Rev. 15; and * Verified compliance with]]
: [[TS]] [[through verification of Mode change checklists, 3-]]
PT-V053C, "Mode Change Checklist Mode 5 to Mode 4," Rev. 12. b. Findings  No findings of significance were identified.
Enclosure 1R22 Surveillance Testing (71111.22 - 5 samples)    a. Inspection Scope  The inspectors witnessed performance of surveillance tests and/or reviewed test data of selected risk-significant structures, systems, and components, to assess whether test results satisfied Technical Specification,
: [[UFS]] [[]]
AR, Technical Requirements Manual, and Entergy procedure requirements. The inspectors verified that:  test acceptance criteria were sufficiently clear; tests demonstrated operational readiness and were consistent
with design basis documentation; test instrumentation had accurate calibrations and appropriate range and accuracy for the application; tests were performed as written; and applicable test prerequisites were satisfied. Following the tests, the inspectors verified that the equipment was capable of performing the required safety functions. The documents reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented five inspection samples, one of which includes
: [[IST]] [[surveillances:  * 3-]]
: [[PT]] [[-R003D, "Safety Injection Test," Rev.29, on April 8, 2009; * 3-PT-R085, "RHR Valves 730 and 731 Disc Integrity Test," Rev 9 (IST); * 3-PT-V032T, "Pressure Decay Test Of Underground Condensate Piping," Rev. 1, conducted on March 22, 2009; *]]
: [[SOP]] [[-]]
: [[RPC]] [[-006A, "Reactor Thermal Power Calculation," Rev. 17, conducted on April 25, 2009; and * 3-PT-R20A, "Auxiliary Boiler Feed Pump Room Temperature Sensors (TC-1112A,]]
: [[TC]] [[-1112S)," Rev. 9, and 3-]]
: [[PT]] [[-R20B, "Auxiliary Boiler Feed Pump Room Temperature Sensors (TC-1113A,]]
: [[TC]] [[-1113S)," Rev. 8, conducted on May 12 - 13, 2009. b. Findings  No findings of significance were identified. 1]]
EP6 Drill Evaluation (71114.06 - 1 sample)    a. Inspection Scope  The inspectors evaluated an emergency classification conducted on June 22, 2009, during a licensed-operator requalification simulator training session. The inspectors observed an operating crew respond to various, simulated initiating events that ultimately resulted in the simulated implementation of the site emergency plan. In particular, the inspectors verified the adequacy and accuracy of the simulated
emergency classification of Site Area Emergency. The inspectors verified this initial classification was appropriately credited as an opportunity toward NRC performance indicator data. The inspectors verified that significant performance deficiencies were appropriately identified and addressed. This evaluation constituted one inspection sample. 


Enclosure 2.
LER
: [[RADIAT]] [[]]
: [[ION]] [[]]
: [[SAFETY]] [[Cornerstone: Public Radiation Safety (]]
PS)  2PS2 Radioactive Materials Processing and Shipping (71122.02 - 6 samples)    a. Inspection Scope  During June 22-26, 2009, the inspectors conducted the following activities to verify that
Entergy's radioactive material processing and transportation programs complied with the requirements of
: [[10 CFR]] [[20, 61, and 71; and Department of Transportation (]]
: [[DOT]] [[) regulations]]
: [[49 CFR]] [[170-189.  (1) The inspectors reviewed the solid radioactive waste system description in the]]
UFSAR, the 2008 radiological effluent release report for information on the types and amounts of radioactive waste disposed, and the scope of the audit program
to verify that it meets the requirements of
: [[10 CFR]] [[20.1101.  (2) The inspectors walked-down the liquid and solid radioactive waste processing systems to verify and assess that the current system configuration and operation agree with the descriptions contained in the]]
UFSAR and in the Process Control
Program (PCP); and reviewed the status of any radioactive waste process equipment that is not operational and/or is abandoned in place; verified that the changes were reviewed and documented in accordance with 10 CFR 50.59, as appropriate. The inspectors reviewed the current processes for transferring and dewatering of radioactive waste resin and sludge discharges into
shipping/disposal containers to determine if appropriate waste stream mixing and/or sampling procedures and methodology for waste concentration averaging provide representative samples of the waste product for the purposes of waste classification as specified in 10CFR61.55 for waste disposal. 
(3) The inspectors reviewed the radio-chemical sample analysis results for each of the radioactive waste streams, reviewed the use of scaling factors and calculations with respect to these radioactive waste streams to account for difficult-to-measure radionuclides, verified that the program assures compliance with
: [[10 CFR]] [[61.55 and 10]]
CFR 61.56 as required by Appendix G of 10 CFR Part
20, and verified that the waste stream composition data accounts for changing operational parameters and thus remains valid between the annual or biennial sample analysis update.  (4) On June 24-25, 2009, Entergy technicians prepared, packaged, and completed shipment No. 09-109 that contained spent filters in a Type A cask for shipment to a waste processor. The inspectors observed Entergy's shipment preparations
that included:  packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifests, shipping papers provided to the driver, and verification of shipment readiness.
Enclosure (5) The inspectors sampled the records of the following non-excepted package shipments to a waste processor, or other entities as applicable, and reviewed these records for compliance with
: [[NRC]] [[and]]
DOT requirements:  * 08-055, Spent fuel pool demineralizers shipment on April 7, 2008; * 08-093, Hudson River silt shipment on May 15, 2008; * 08-170, Sodium hydroxide shipment on September 4, 2008; * 08-200, Unit 1 debris shipment on November 4, 2008 * 08-223, Fuel sipping equipment shipment to Westinghouse on December 15, 2008; * 09-068, Dry active waste shipment on April 15, 2009; * 09-100, Unit 1 pool sludge shipment on June 10, 2009; * 09-102, Unit 2 primary resin shipment on June 17, 2009; * 09-103, Unit 3 bead resin shipment on June 17, 2009; and * 09-109, Spent filter shipment on June 25, 2009.  (6) The inspectors reviewed Entergy's Licensee Event Reports, Special Reports, audits, State agency reports, and self-assessments related to the radioactive material and transportation programs performed since the last inspection and
determined that identified problems are entered into the corrective action program for resolution. The inspectors also reviewed corrective action reports written against the radioactive material and shipping programs since the previous inspection.
b. Findings  No findings of significance were identified. 4.
: [[OTHER]] [[]]
ACTIVITIES
4OA1 Performance Indicator Verification  Resident Inspector Baseline Inspection (71151 - 2 samples)
a. Inspection Scope  The inspectors reviewed the performance indicator data listed below, which is associated with the Barrier Integrity and Mitigating Systems cornerstones, respectively. The inspectors used Nuclear Energy Institute 99-02, "Regulatory Assessment
Performance Indicator Guideline," Rev. 5, and applicable Entergy procedures to verify individual performance indicator accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment.  * Reactor Coolant System Specific Activity (April 2008 to March 2009) * Safety System Functional Failure (April 2008 to March 2009)
Enclosure  b. Findings  No findings of significance were identified.
: [[4OA]] [[2 Identification and Resolution of Problems (71152 - 3 samples)  .1 Routine Problem Identification and Resolution (]]
PI&R) Program Review    a. Inspection Scope  As required by Inspection Procedure 71152, "Identification and Resolution of Problems," and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergy's corrective action program. The review was accomplished by accessing Entergy's computerized database for condition reports, and attending condition report screening meetings.
In accordance with the baseline inspection procedures, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for further follow-up and review. The inspectors assessed Entergy personnel's threshold for problem identification, the adequacy of the cause
analysis, extent of condition reviews, operability determinations, and the timeliness of the associated corrective actions. The condition reports reviewed during this inspection are listed in the applicable inspection sections. b. Findings  No findings of significance were identified.  .2 Public Radiation Safety Cornerstone
a. Inspection Scope  The inspectors screened 33 corrective action condition reports initiated between January 2008 and June 2009 and associated with the radiological waste transportation program. b. Findings  No findings of significance were identified.  .3 Focused Review of Corrective Actions Related to the Installation and Project Management of the New Alert and Notification System (ANS) (71152 - 1 sample)
a. Inspection Scope  The inspectors reviewed Entergy personnel=s actions in response to condition reports (CRs) generated as a result of issues associated with the installation and project management of the new alert and notification system (ANS) for the Indian Point Energy Center. The inspectors also reviewed Entergy procedures on project management and
Enclosure external stakeholder communications. In addition, the inspectors interviewed applicable members of Entergy's staff including a lead project manager and licensing staff. The focus of this inspection was to verify that the corrective actions, reviewed during the December 2008 Enforcement Follow-up Inspection (Inspection Procedure 92702,
: [[NRC]] [[Inspection Report 50-247/286, 2008503, dated January 27, 2009,]]
: [[ADAMS]] [[Accession No.]]
: [[ML]] [[090280267), were being completed in a thorough and timely manner. b. Findings  No findings of significance were identified. The inspectors reviewed]]
: [[CR]] [[s documenting issues related to the installation and project management of the new]]
ANS placed into service for the Indian Point Energy Center in 2008. Entergy staff has taken appropriate corrective actions, or has corrective actions planned to address each issue that was identified. For example, inspectors verified that responsible personnel have taken corrective actions, or have corrective actions planned to revise their project management process, require greater senior management oversight for projects, and develop a new
procedure for interactions with external stakeholders.  .4 Semi-Annual Trend Review: Human Performance - Error Prevention Techniques (71152 - 1 sample)
a. Inspection Scope  In July 2009, inspectors reviewed Entergy staff's progress in implementing corrective actions identified in 2008 to address Human Performance issues as outlined in Entergy's Human Performance Improvement Plan with a focus on specific efforts since January
2009. The inspectors evaluated staff performance improvement plans and actions using inspection guidance in Inspection Procedure 71152, "Identification and Resolution of Problems."  Specifically, the inspectors assessed Entergy's progress in addressing human performance by evaluating whether Entergy's internal milestones were being monitored and consistently met and whether adjustments in approach were made when
necessary. This inspection focused on the actions implemented since January 2009. The inspectors conducted a review of the applicable condition reports (CRs), corrective action assignments (CAs), focused self-assessments, Quality Assurance group assessments, and causal evaluations for human performance events and errors. The
inspectors also reviewed Entergy internal performance indicators related to their performance improvement plan, and reviewed a sample of revised procedures in order to assess the adequacy of the performance plan and effectiveness of corrective actions. b. Findings and Observations  No findings of significance were identified.
In late December 2008, NRC inspectors independently reviewed the causal evaluation and corrective actions focused on an emerging trend, identified by Entergy personnel, and associated with human performance errors. Entergy staff and managers identified several events, attributable to human performance errors that occurred at Indian Point
(both units) in 2008, which resulted in personal injury and/or equipment failures. The
Enclosure inspectors determined that Entergy managers recognized this adverse trend in human performance, and developed a Human Performance Program to address the causes of the events, and to assist in the prevention or mitigation of future occurrences. The inspectors noted that the Human Performance Program included actions to understand
the causes of human performance errors, to reduce these human performance errors in the future, and to monitor future performance. The inspectors determined Entergy staff and managers developed station-wide communication tools, training plans, and adjusted the site business plan to address
these common causes of human performance errors. New communication tools developed included Safety and Human Performance Stand Downs and periodic human performance bulletins. The Safety and Human Performance Stand Downs were used to develop a forum to reinforce site human performance expectations and discuss recent human performance error events. Entergy managers also scheduled future stand downs to coincide with major evolutions on site in 2009, such as the Unit 3 refueling outage.
The inspectors noted that Entergy staff developed a Human Performance Simulator and Work Management Academy to provide training on human performance traps, human performance tools, and to improve work planning and execution. The Human Performance Simulator focuses on reinforcing the proper threshold for identifying error traps and the effective use human performance tools to accomplish tasks. Operations
and maintenance departments have completed this training, and it will now be included as annual refresher training for their department personnel. The Work Management Academy was required for all supervisory personnel and reinforced Entergy's work management model and procedures. Entergy staff and managers also developed its Thought Improvement Process (TIP) Initiative to encourage employees to provide
constructive feedback to improve the site's human performance. The inspectors also noted that Entergy staff and managers established commitments to monitor future human performance at Indian Point. In particular, human performance indicators and self-assessment results would be used to monitor the effectiveness of the
current programs and for evaluation of future trends in human performance. The inspectors concluded that Entergy managers took action to address the site's emerging adverse human performance trend. The programs established within Entergy's Human Performance program were determined to be reasonable to address the recent human performance.
During the July 2009 semi-annual trend review, inspectors determined that Entergy staff continued to make progress in implementing their corrective action plans to address human performance issues related to error prevention and to make adjustments to those actions based on the results of self-assessments, performance indicators, and benchmarking. For example, based on observations of supplemental workers during the recent Unit 3 refueling outage, actions were being developed to provide additional
oversight of supplemental workers. The inspectors also noted that, in accordance with previous corrective actions, Entergy staff and managers had:  * Continued to use the Human Performance Simulator to train various departments, and to check and adjust development of dynamic learning activities in the simulator;
Enclosure * Implemented a standard schedule for site wide stand downs during outage and non-outage periods;  * Revised pre-job briefing procedures to include signature accountability, * Implemented a task/job observation program aligned with the work control process and Most Error Likely Task-focused crew assessments;  * Assigned experienced mechanics, technicians, and operators to procedure groups;  * Reinforced critical procedure steps through the use of special markings, briefs, and feedback;  * Filled key personnel vacancies previously identified as necessary to strengthen the organization's effectiveness in preventing human error;  * Improved adherence to online and outage work management milestones;  * Improved effectiveness of work package walk downs and feedback;  * Established weekly work package quality meetings. Additionally, the inspectors noted that Entergy has developed additional performance indicators to assist in monitoring progress in addressing human errors, and is planning to
conduct annual Human Performance training to first-line supervisors and above. The recent trend in human performance related to error prevention indicated that corrective actions, to date, have not resulted in a decrease in the human error rate trend, primarily due to issues that occurred during the Unit 3 refueling outage.
Notwithstanding, the inspectors concluded that station management has adjusted its actions/focus as a result of its evaluation of additional performance information, especially from the outage. The programs and actions established within Entergy's Human Performance program were determined to be reasonable to address the recent human performance issues related to error prevention.
.5 Focused Review of Corrective Actions for 31 Emergency Diesel Generator Fuel Oil Control Valve Maintenance Issues (71152 - 1 sample)    a. Inspection Scope  The inspectors reviewed Entergy's corrective actions to address inadequate maintenance associated with the 31 emergency diesel generator (EDG) detailed under condition report
: [[CR]] [[-]]
IP3-2008-02508, dated October 9, 2008. The inspectors evaluated the apparent cause evaluation to ensure the identified causes and corrective actions
were adequate and appropriate for the circumstances, as well as commensurate with the safety significance applicable to the highly risk significant EDGs. b. Findings and Observations  No findings of significance were identified.
However, the inspectors identified the apparent cause evaluation (ACE) did not address a work control issue. Specifically, the inspectors concluded the evaluation team did not fully consider that Entergy personnel planned and performed this maintenance under the minor maintenance work control process contrary to Entergy work control procedures.
Enclosure  The inspectors determined that the Entergy work control procedures, detailed in
: [[EN]] [[-]]
: [[WM]] [[-100, "Work Request (WR) Generation, Screening and Classification," and]]
: [[EN]] [[-]]
WM-105, "Planning," identify that detailed work instructions are required for those work
activities that are risk significant and require entry into limiting conditions for operation. In accordance with these procedures, more detailed work instructions should have been generated to ensure the work activity associated with the 31 EDG was appropriate for the circumstances. In particular, contrary to the above procedures, the minor maintenance work package did not contain adequate instructions regarding the
operation and maintenance of the fuel oil pressure control valve (PCV),
: [[PCV]] [[1247, for the 31]]
: [[EDG.]] [[The instructions did not provide for details regarding the gasket replacement and its effect on the]]
: [[PCV]] [[internal settings. As a result, maintenance workers were not cognizant of]]
: [[PCV]] [[internal setting changes during the gasket replacement which, ultimately, resulted in the]]
: [[31 EDG]] [[not being able to provide appropriate fuel oil pressure to meet surveillance and operational requirements during the post-maintenance testing, and required a premature shutdown of the]]
EDG, as well
as accrual of additional out-of-service hours. The inspectors determined that the performance of maintenance on the 31 EDG, using a minor maintenance work package contrary to established work control procedures was a violation. However, because the equipment issue was identified by Entergy personnel
prior to the completion of the overall maintenance window, the inspectors determined that in accordance with
: [[IMC]] [[0612, Appendix E (Section 5), the performance issue is considered a "work-in progress" issue that is of minor significance. As a result, this failure to comply with Entergy work control procedures constitutes a violation of minor significance that is not subject to enforcement action in accordance with the]]
NRC's
Enforcement Policy. Entergy personnel entered this issue in the corrective action program (CR-IP3-2009-02958). 4OA3 Event Follow-up (71153 - 4 samples) 
.1 Unintended
: [[RCS]] [[leak initiated on April 1, 2009, during fuel load with]]
RCS at >90 ft  a. Inspection Scope  The inspectors evaluated Entergy staff's response to an unintended RCS leak initiated
when supplemental maintenance workers commenced work to replace the packing in valve
: [[SP]] [[-954A, a sampling system root stop isolation valve from the 31]]
: [[RCS]] [[hot leg. Specifically, the inspectors reviewed Entergy staff's response to the event and reviewed the conditions that led to the event to evaluate if additional inspection was required, and to ensure that Entergy personnel properly classified the event. The inspectors verified Entergy's corrective actions were appropriate in response to the event. This issue was initially entered into Entergy's corrective action program as]]
: [[CR]] [[-]]
IP3-2009-01550 with a
follow up entry as
: [[CR]] [[-]]
IP3-2009-03003.   


Enclosure  b. Findings  Introduction:  The inspectors identified a
Technical Specification Prohibited
: [[NCV]] [[of very low safety significance (Green) of 10]]
CFR 50.65(a)(4) because Entergy personnel did not adequately assess and manage
the risk associated with planned corrective maintenance. Specifically, Entergy personnel did not include the increase in shutdown plant risk in its risk assessment and use appropriate mitigating strategies while repacking SP-954A during fuel reload operations.
Description:  On April 1, 2009, Indian Point Unit 3 was in a shutdown condition for refueling outage 3R15. The plant was in Mode 6, "Refueling," with reactor core reload in progress, and the refueling cavity was flooded to approximately 93', as required to support fuel movements. The inspectors noted that maintenance personnel were assigned to perform work order (WO) 51483809, Task 1, "Packing Leak Noted During
: [[PT]] [[-R131,]]
RCS Integrity Test, SP-
954A Packing Leak During
: [[PT]] [[-R131]]
: [[RCS]] [[Integrity Test," with a site radiological protection (RP) technician providing radiological support. To replace the valve's packing, the]]
: [[WO]] [[directed the workers to remove the valve's bonnet and internals. This valve is a root stop isolation valve for a sample system line from the 31 reactor coolant system (]]
RCS) loop, and is not isolable from the
: [[RCS.]] [[Upon removal of the valve's bonnet, the maintenance and]]
: [[RP]] [[technician noticed an unexpected amount of water coming from the inside of the valve. The maintenance and]]
RP technician promptly replaced the valve bonnet in order to stop the leak, which was later estimated at approximately one liter of RCS water. The inspectors determined that
this condition represented an uncontrolled leak in the
: [[RCS]] [[and noted that no individual was contaminated as a result. During the review of this condition, the inspectors noted that the repacking of]]
SP-954A was originally scheduled to be conducted by Entergy personnel on March 27, 2009,
while the
: [[RCS]] [[was in a drained-down condition, with refueling cavity/]]
: [[RCS]] [[water level at 61' 8", with no fuel in the reactor vessel. The inspectors noted that]]
: [[SP]] [[-954A is physically located at the mid-level position on the 31]]
RCS hot leg, which is approximately at the 62' elevation. Due to work backlogs, this maintenance item was transferred to supplemental personnel for completion on March 29, 2009. However, it
was identified that the work activity required the installation of scaffolding to perform the maintenance, which further delayed the work until April 1, 2009. Since this work item did not have the proper logic ties in the outage schedule to the original, drained-down and defueled condition, the subsequent delays in the actual start of this work activity resulted in the work being performed after the reactor cavity was re-flooded to support fuel reload.
Entergy personnel utilize procedure
: [[IP]] [[-]]
: [[SMM]] [[-OU-104, "Shutdown Risk Assessment" to ensure requirements of]]
: [[10 CFR]] [[50.65, "Requirements for monitoring the effectiveness of maintenance at nuclear power plants" are met during plant shutdown conditions.]]
IP-SMM-OU-104 requires the Outage Risk Assessment Team (ORAT) to review the outage schedule prior to shutdown to assess the sequencing of events and document any errors
within the schedule. Additionally, the
: [[OR]] [[]]
AT is required to document their review and all
Enclosure resolutions to errors that had been identified within the schedule in a condition report prior to the commencement of the outage. In the 3R15 Refueling Outage Schedule Risk Assessment Report, the
: [[OR]] [[]]
AT identifies that a drain-down to 61' 8" was to occur on March 27, 2009, to support work activities associated with the 31 reactor coolant pump
(RCP), and did not describe work to be performed on
: [[SP]] [[-954A. Furthermore, the]]
ORAT review of the outage schedule did not identify that the proper logic ties, which would have prevented the valve repack work from drifting out of the appropriate drain down window, were not in place for WO 51483809.
The inspectors reviewed Entergy staff's root cause analysis (RCA) of the event, which detailed two root causes and three contributing causes associated. Specifically, the root causes were determined to be:  (1) Failure to Comply With (Tag out) Procedural Requirements, and (2) Inadequate Tag Out to Ensure Worker Protection. The contributing causes were determined to be:  (1) Inadequate Commitment to Outage Preparation, (2) Missed Opportunity in Scheduling Work, and (3) Missed Opportunity to Identify Inappropriate Plant Conditions for Scope of Work During Pre-job Briefs.
Consistent with these contributing causes, the inspectors determined that Entergy personnel did not identify their failure to properly assess and manage the risk associated with the SP-954A valve work prior to outage 3R15, and during opportunities within the outage process that occurred following the originally-scheduled start date of March 27th, e.g., (1) work backlog that transferred the activity to supplemental personnel, (2) the
delay to build scaffolding, and (3) the actual day the work started. Analysis:  The inspectors determined there was a performance deficiency because Entergy staff did not completely and accurately assess and manage the increase in plant risk resulting from planned maintenance activities.
The inspectors determined that this finding affected the Initiating Event cornerstone and was more than minor because Entergy staff's risk assessment did not consider maintenance activities that could increase the likelihood of initiating events. The inspectors determined the significance of this finding using IMC 0609, Appendix G,
"Shutdown Operations Significance Determination Process."  The inspectors determined this finding was of very low safety significance (Green) because Entergy personnel maintained required mitigation capability in accordance with IMC 0609 Appendix G, Attachment 1, Checklist 4.
The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance, because Entergy personnel did not appropriately plan work activities by incorporating appropriate risk insights, job site conditions, contingencies, and abort criteria consistent with nuclear safety.  (H.3(a))  Enforcement:  10 CFR 50.65(a)(4), requires, in part, that licensees assess and manage the increase in risk that may result from proposed maintenance activities. Contrary to
the above, prior to and during the 3R15 refueling outage, Entergy personnel did not adequately assess and manage the increase in risk associated with the packing replacement on
: [[SP]] [[-954A, the 31]]
: [[RCS]] [[hot leg sample root isolation valve, which is unisolable from the]]
: [[RCS.]] [[Specifically, Entergy personnel did not identify the full impact the]]
SP-954A work had on nuclear safety, i.e., a possible unmonitored/uncontrolled leak
in the RCS, and take appropriate actions to control the maintenance. Because this
Enclosure violation is of very low safety significance and has been entered into the Entergy's corrective action program as
: [[CR]] [[-]]
: [[IP]] [[3-2009-03003, this violation is being treated as an]]
: [[NCV]] [[, consistent with Section]]
: [[VI.A.]] [[1 of the]]
: [[NRC]] [[Enforcement Policy. (]]
NCV 05000286/2009003-01: Failure to assess and manage the increase in risk prior to
the performance of maintenance on valve that was unisolable from the reactor coolant system)
.2 Manual Reactor Trip on May 15, 2009 (3FO9A)
a. Inspection Scope  The inspectors evaluated the response of control room personnel following the manual reactor trip that was initiated due to steam generator water levels that approached automatic reactor trip setpoints. The inspectors reviewed plant computer data, which included the sequence of events report and plant parameter traces, and discussed the event with plant personnel, to verify that plant equipment responded as expected, and to
ensure that operating procedures were appropriately implemented. The inspectors verified that Entergy's post-trip review group (PTRG) correctly identified the cause(s) of the trip to ensure appropriate corrective actions were implemented prior to restart. This event and the
: [[PTRG]] [[report were entered into Entergy's corrective action program as]]
: [[CR]] [[]]
: [[IP]] [[3-2009-02368. The inspectors reviewed the following]]
NRC Operating Experience
information for applicability:  Review of Operating Experience Smart Sample: OpESS
: [[FY]] [[2009-02, "A Negative Trend and Recurring Events Involving Feedwater Systems."    b. Findings  Introduction:  The inspectors identified a self-revealing finding of very low safety significance (Green) because Entergy personnel did not have adequate procedures for the circumstances for maintenance associated with air-operated valves. Specifically, existing Entergy maintenance procedures did not ensure that the 33 steam generator (]]
SG) feedwater regulating valve (FRV) positioner feedback arm connecting linkage
hardware were properly secured following maintenance. As a result, on May 15, 2009, this linkage became disconnected which led to
: [[SG]] [[level oscillations that required a manual reactor trip by control room operators. Description:  On May 15, 2009, Unit 3 control room operators responded to]]
: [[SG]] [[water level deviation alarms and took manual control of the]]
: [[FRV]] [[as required by procedures. When operators did not observe a response in main feedwater flow or]]
SG water level, operators manually tripped the reactor prior to automatic reactor protection setpoints being reached. Subsequently, Entergy personnel identified that feedback linkage (threaded rod between swivel-joints) between the valve actuator and the valve positioner for FCV-437 had disconnected, and that a locking nut on the threaded rod portion had backed off, which was an unexpected condition. A post-transient review team was
initiated, as well as a root cause evaluation, to determine the cause of the event. In addition, Entergy personnel performed an initial extent-of-condition review to determine the condition of other valve positioners that may present similar operability or functionality concerns. The inspectors noted that Entergy personnel completed the post-transient review, performed repairs on the
: [[33 FRV]] [[, as well as the 31]]
FRV, due to
Enclosure concerns regarding the conduct of maintenance on both valves during the recent refueling outage that ended in April 2009. The inspectors reviewed the root cause analysis (RCA), which was conducted under
condition report
: [[CR]] [[-]]
: [[IP]] [[3-2009-02368. The inspectors noted that Entergy personnel had determined the cause of the event to be inadequate procedure directions and written instructions, with one of the contributing causes attributed to ineffective use of human performance tools. Specifically, the governing maintenance procedure for the]]
: [[FRV]] [[s, 0-]]
VLV-416-AOV, did not have appropriate guidance for the proper installation and
tightening of locknuts for the feedback linkage. Additionally, the
: [[RCA]] [[identified that the]]
FRV diagnostic testing procedure, 0-VLV-404-AOV, which followed the performance of the overhaul and maintenance of the valve during the most-recent refueling outage, required a specific "inspection" be performed under the calibration/post-maintenance section of this procedure. In Attachment 5, the technician is required to inspect the feedback linkage to ensure jam nuts on the threaded rod are tight. The RCA detailed that this "inspection" provided an opportunity for confusion because it did not explicitly
define the inspection attribute of "tight."  The RCA also detailed a missed opportunity in that the technician did not observe that the upper jam nut on the threaded rod of the feedback linkage was missing. While the inspectors determined that this lockwasher was most likely not installed during
original installation during the preceding refueling outage in 2007, the inspectors concluded that it should have been identified during the most recent 2009 outage, because the remaining FRVs on both units have lockwashers installed on both ends of the threaded rods. Moreover, operating experience located within the governing procedures, which are also required to be discussed during pre-job briefs, identify the
different failure mechanisms of air-operated valves in high vibration environments. Some of these failures address the proper tightening and installation of jam nuts or appropriate locking mechanisms to prevent similar occurrences, which in turn, should have sensitized the technicians to these issues to ensure jam nuts encountered during these maintenance opportunities were appropriately tightened.
The inspectors also noted that the maintenance and diagnostic procedures were reviewed under the Procedure Upgrade Project (PUP). This project was instituted by Entergy personnel in response to identified deficiencies in procedures that manifested into inspection findings in previous assessment periods, and a classification of a
substantive cross-cutting issue that warranted Entergy's establishment of the PUP to improve the quality of procedures at both Units No. 2 and 3. Analysis: The inspectors determined there was a performance deficiency because Entergy did not have adequate maintenance procedures to ensure for positive locking of connecting hardware for air-operated valve positioner feedback linkages. The inspectors concluded the finding is more than minor because the finding was associated
with the equipment performance attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the inadequate procedures resulted in the failure of a non-safety-related portion of FCV-437, the 33 steam generator main feedwater regulating
valve, and resulted in a manual reactor trip due to steam generator water levels that
Enclosure approached automatic reactor trip protection actuation setpoints. The inspectors evaluated the finding using IMC 0609, Attachment 4, "Initial Screening and Characterization of Findings," and determined the finding did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would
not be available. Consequently, the finding is of very low safety significance (Green). The inspectors determined that this finding had a cross-cutting aspect in the area of Human Performance because Entergy personnel did not ensure that complete, accurate and up-to-date procedures were available to perform appropriate maintenance on air-
operated valve positioners associated with the
: [[33 SG]] [[]]
FRV.  (H.2(c)). Enforcement: Enforcement action does not apply because the performance deficiency was related to non-safety related equipment and procedures and did not involve a violation of regulatory requirements. Because this finding does not involve a violation of regulatory requirements and has very low safety significance, this issue is being treated
as a
: [[FIN.]] [[]]
FIN 05000286/2009003-02:  Inadequate maintenance procedures on FRVs resulted in a manual reactor trip. 
.3 Automatic Reactor Trip on May 28, 2009 (3FO9B)    a. Inspection Scope
The inspectors evaluated the response of control room personnel following the automatic reactor trip that occurred following the down power to 65% in response to increasing vibrations on the 32 main boiler feed pump on May 25, 2009. The inspectors reviewed plant computer data, evaluated plant parameter traces, and discussed the event with plant personnel, to verify that plant equipment responded as expected, and to
ensure that operating procedures were appropriately implemented. The inspectors verified that Entergy's post-trip review group (PTRG) correctly identified the cause(s) of the trip to facilitate corrective actions prior to restart. This event and the
: [[PTRG]] [[report were entered into Entergy's corrective action program as]]
CR IP3-2009-02494. Corrective actions included repair to both the 31 and 32 main boiler feed pumps as well
as a Root Cause Analysis (RCA) to determine the cause(s) of the feed pump failures, due July 9, 2009. b. Findings  No findings of significance were identified.  .4 Pressurizer Pressure Low Pressure and Instrument Failure Condition on June 10, 2009    a. Inspection Scope  The inspectors evaluated the response of control room personnel following the receipt of
a low pressurizer pressure alarm, along with minor turbine power and load oscillations that were observed on June 10, 2009. The inspectors reviewed plant computer data, evaluated plant parameter traces, discussed the condition with plant personnel, and verified that plant equipment responded as expected. The inspectors reviewed 3-AOP-INST-1, "Instrument/Controller Failures," Rev. 5, to verify that required actions were
Enclosure completed. The inspectors also reviewed the details of this condition as documented in the corrective action program under condition report
: [[CR]] [[-]]
IP3-2009-02680. b. Findings  No findings of significance were identified. 4OA5 Other Activities  Quarterly Resident Inspector Observations of Security Personnel and Activities    a. Inspection Scope  During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that these activities were consistent with Entergy security procedures and applicable regulatory requirements. Although these
observations did not constitute additional inspection samples, the inspections were considered an integral part of the normal, resident inspector plant status reviews during implementation of the baseline inspection program. b. Findings  No findings of significance were identified. 4OA6 Meetings, including Exit  Exit Meeting Summary  On July 22, 2009, the inspectors presented the inspection results to Mr. Joseph Pollock and other Entergy staff members, who acknowledged the inspection results. While some proprietary items were reviewed and returned during the inspection, no proprietary
information is presented in this report.
: [[ATTACH]] [[]]
: [[MENT]] [[:]]
: [[SUPPLE]] [[]]
: [[MENTAL]] [[]]
: [[INFORM]] [[]]
: [[ATION]] [[Attachment]]
: [[SUPPLE]] [[]]
: [[MENTAL]] [[]]
: [[INFORM]] [[]]
: [[ATION]] [[]]
: [[KEY]] [[]]
: [[POINTS]] [[]]
: [[OF]] [[]]
CONTACT
Entergy Personnel  J. Pollock, Site Vice President A. Vitale, General Manager, Plant Operations K. Davison, Assistant General Manager, Plant Operations P. Conroy, Director, Nuclear Safety Assurance
D. Gagnon, Manager, Security R. Walpole, Manager, Licensing B. Beckman, Manager, Maintenance J. Dinelli, Assistant Operations Manager, Unit 3 V. Myers, Supervisor, Mechanical Design Engineering  T. Orlando, Engineering Director R. Burroni, Manager Programs, Components and Engineering
: [[D.]] [[Loope, Manager, Radiation Protection S. Verrochi, Manager System Engineering F. Inzirillo, Manager, Quality Assurance N. Azevedo, Supervisor, Code Programs T. Morzello, Maintenance Supervisor]]
: [[G.]] [[Dahl, Licensing Engineer H. Anderson, Licensing Engineer D. Smith,]]
: [[ALARA]] [[Specialist G. Hocking, Supervisor, Radiation Protection Support R. Blaine, Supervisor, Radiation Protection Operations]]
: [[S.]] [[Sandike, Specialist, Effluent & Environmental Monitoring P. Donahue, Specialist, Effluent & Environmental Monitoring R. Mages,]]
: [[ALARA]] [[Specialist]]
: [[N.]] [[Papayia,]]
QA B. Allen, Code Programs
R. Walpole, Manager, Licensing M. Burney, Licensing
Attachment
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ITEMS]] [[]]
: [[OPENED]] [[,]]
: [[CLOSED]] [[]]
: [[AND]] [[]]
: [[DISCUS]] [[]]
SED  Open and Closed  05000286/2009003-01 NCV  Failure to assess and manage the increase in risk
prior to the performance of maintenance on valve      that was unisolable from the reactor coolant      system. (Section
: [[4OA]] [[3.1)  05000286/2009003-02]]
FIN  Inadequate maintenance procedures on FRVs
resulted in a manual reactor trip.  (Section
: [[4OA]] [[3.2)]]
: [[LIST]] [[]]
: [[OF]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Section 1R01:  Adverse Weather Protection  Procedures Engineering Guide]]
: [[ENN]] [[-]]
: [[EP]] [[-G-004, Switchyard and Large Power Transformer Preventive Maintenance Guidelines, Rev. 0 3-SOP-EL-005, Operation of On-Site Power Sources, Rev.]]
: [[38 IP]] [[-]]
SMM-OP-104, Offsite Power Continuous Monitoring and Notification, Rev. 8 0-MS-412, Inspection and Cleaning of Bus Bars, Contacts, Ground Connections, Wiring and Insulators, Rev. 0  Work Orders 52186394-01 00116598 186960 00132918 00177978 00189376 51690233-01 51694953-01 00172295
Condition Reports (CR-IP3-) 2008-01498 2009-02261 2009-02241 2009-01347 2009-01606 2009-02799 2009-02666 2009-02749 2005-02634
Work Requests 00131842  Drawings 9321-F-31153, Conduit Details Manhole 34, Rev. 8


Section 1R04:  Equipment Alignment
Condition Due to a Surveillance
Procedures
: [[SOP]] [[-]]
FW-004, Auxiliary Feedwater System Operation, Rev. 24 3-COL-EL-005, Diesel Generators, Rev. 34
Work Orders 51675356 00131842   


Attachment Section 1R05:  Fire Protection
Requirement Never Performed for
Procedures
: [[EN]] [[-]]
: [[DC]] [[-161, Control of Combustibles, Rev.]]
: [[3 IP]] [[-]]
: [[SMM]] [[-DC-901,]]
: [[IP]] [[]]
EC Fire Protection Program, Rev. 6
Other
: [[EN]] [[-]]
DC-189, Fire Drills, Rev. 1 Fire Brigade Drill Report dated June 10, 2009  Section 1R11: Licensed Operator Requalification
Procedures
: [[EOP]] [[-E-0, Reactor Trip or Safety Injection]]
: [[FR]] [[-H.1, Response to Loss of Heat Sink  Other]]
: [[13SX]] [[-]]
LOR-SES003, Miscellaneous Equipment Failures and Events, Rev. 0


Section 1R12:  Maintenance Effectiveness
the Atmospheric Steam Dump Valve  
Procedures 3-PT-Q016,
: [[EDG]] [[and Containment Temperature]]
: [[SW]] [[Valves]]
: [[SWN]] [[-1176 & 1176A and]]
SWN-TCV-1104 & 1105, Rev. 20  Condition Reports (CR-IP3-) 2009-00730 2009-01936 2009-01999 2009-02578
Maintenance Rule Monitoring Documents
: [[EN]] [[-]]
: [[DC]] [[-143, System Health Reports, Rev.]]
: [[8 EN]] [[-]]
: [[DC]] [[-159, System Monitoring Program, Rev.]]
: [[3 EN]] [[-]]
: [[DC]] [[-167, Classification of Structures, Systems, and Components, Rev.]]
: [[2 EN]] [[-]]
: [[DC]] [[-203, Maintenance Rule Program, Rev. 1]]
: [[EN]] [[-]]
: [[DC]] [[-204, Maintenance Scope and Basis, Rev.]]
: [[1 EN]] [[-]]
: [[DC]] [[-205, Maintenance Rule Monitoring, Rev.]]
: [[2 EN]] [[-]]
: [[DC]] [[-206, Maintenance Rule (a)(1) Process, Rev.]]
: [[1 SED]] [[-]]
AD-22, Condition Monitoring of Maintenance Rule Structures, Rev. 4
Miscellaneous Maintenance Rule Basis Document - Main Feedwater System  Work Orders 51559321 00191318 51484856 00196649 5202207 00138837 00187790 00171345 51559321 00154220 00166500  Section 1R13:  Maintenance Risk Assessment and Emergent Work Control  Procedures
: [[IP]] [[-]]
SMM-WM-101, On-Line Risk Assessment, Rev. 3 Work Week Managers Operator's Risk Reports
3R15 Refueling Outage Schedule Risk Assessment Report, Amended Feb. 2009
Attachment
: [[IP]] [[-]]
SMM-OU-104, Attachment 9.1, Shiftly Outage Shutdown Safety Assessment, Rev. 5
Section 1R15:  Operability Evaluations
Procedures
: [[EN]] [[-]]
OP-104, Operability Determinations, Rev. 3
Indian Point Unit 3 Updated Final Safety Analysis Report, Rev. 2 3-SOP-ESP-001, Local Equipment Operation and Contingency Actions, Rev. 19 0-TUR-403-AFP, Worthington Auxiliary Boiler Feed Pump Turbine Preventive Maintenance, Rev. 3
Condition Reports (CR-IP3-) 2009-01829  Other Documents WO 00190284-01 167459-01 51559347-05/12/13 00167459-03  Section 1R18: Plant Modifications
Procedures 3-NF-321, Incore Thermocouple Wide Range
: [[RTD]] [[and Narrow Range]]
: [[RTD]] [[Measurement, Rev.]]
: [[0 SOP]] [[-]]
RCS-015, Operation of the Inadequate Core Cooling Monitor System, Rev. 7 and 8
Drawings (9321-F-) 95273  95283  95293  36853  Condition Reports
: [[CR]] [[-]]
: [[IP]] [[3-2009-01893  Other Engineering Change]]
: [[EC]] [[-14450, Core Exit Thermocouple]]
CE-T-49 (H05) Substitution
Work Orders  51559602-01 51692338-01 51692339-01  Section 1R19:  Post-Maintenance Testing
Procedures
: [[EN]] [[-]]
: [[MA]] [[-101, Conduct of Maintenance, Rev.]]
: [[6 EN]] [[-]]
: [[WM]] [[-102, Work Implementation and Closeout, Rev.]]
: [[2 EN]] [[-]]
WM-105, Planning, Rev. 5 0-VLV-431-PAC, Valve Repacking With or Without Live Loading, Rev. 1
Condition Reports (CR-IP3-) 2009-01903  Work Orders 00190295 00161170 00191706 52022852


Attachment Section 1R20:  Refueling and Outage Activities
Local Nitrogen Controls (Section  
Procedures 0-VLV-413-MOV, Motor Operated Valve Minor Preventive Maintenance, Rev. 4 3-PT-R035G, Leakage Test for
: [[SI]] [[_]]
MOV-885A Valve Container (Mini Containment), Rev. 3 3-POP-1.3, Plant Startup From Zero to 45% Power, Rev. 54
3-POP-2.1, Operation at Greater Than 45% Power, Rev. 53 3-POP-3.3, Plant Cooldown - Hot To Cold Shutdown, Rev. 49 3-POP-4.1, Operation at Cold Shutdown, Rev. 28 3-SOP-RHR-001, Residual Heat Removal System Operation, Rev. 40 3-SOP-CVCS-003, Reactor Coolant System Boron Concentration Control, Rev. 36
3-POP-3.2, Plant Recovery From Trip, Hot Standby, Rev. 0 3-POP-1.2, Reactor Startup, Rev. 50 3-SOP-FW-001, Main Feedwater System Operation, Rev. 51  Miscellaneous
: [[WO]] [[51560024  Section 1R22:  Surveillance Activities  Miscellaneous Calculation]]
: [[IP]] [[-CALC-08-00111 (Engineering Change]]
: [[EC]] [[-9070) Exelon Certificate of Calibration No. 0010523170 (Fluke No.]]
IP3 IC-1547)
Drawing 9321-H-56293, Aux. Feedwater Building Temp. Switch Support details, Rev. 0 Drawing 9321-LL-31313, Schematic Diagram Miscellaneous Solenoid Valves, Rev. 4 Drawing 9321-LL-31343, Schematic Diagram Supervisory Annunciator, Rev. 22  Work Orders 51550367 51483627 51688528 51687447  Section
: [[2PS]] [[2:  Radioactive Material Processing and Transportation  Procedures  Process Control Program,]]
: [[EN]] [[-RW-106, Rev. 1  Radioactive Shipping Procedure,]]
: [[EN]] [[-]]
: [[RW]] [[-102, Rev. 6 14-170 and 8-120 Cask/Liner Handling Procedure,]]
: [[VY]] [[-]]
OPF 2511, Rev. 42


Section 4OA1:  Performance Indicator Verification
4OA3)
Procedures
: [[EN]] [[-]]
: [[LI]] [[-114, Performance Indicator Process, Rev.]]
: [[4 EN]] [[-]]
: [[LI]] [[-114, Attachment 2,]]
: [[NRC]] [[Performance Indicator Technique Sheet, Rev. 2, for First Quarter 2008 thru Fourth Quarter 2008 for selected Performance Indicators]]
: [[EN]] [[-LI-106, Attachment 9.4,]]
: [[NRC]] [[Submittal Review, Rev. 3]]
: [[NEI]] [[99-02, Regulatory Assessment Performance Indicator Guideline, Rev. 5]]
: [[EN]] [[-]]
LI-144, Performance Indicator Process, Rev.3, Attachment 9.2  Other NRC Performance Indicator Technique/Data Sheets 


Attachment Condition Reports (CR-IP3-) 2009-0690 2009-2868  Section
==LIST OF DOCUMENTS REVIEWED==
: [[4OA]] [[2:  Identification and Resolution of Problems  Procedures]]
: [[EN]] [[-DC-114, Project Management, Rev.]]
: [[9 EN]] [[-]]
: [[HU]] [[-104, Engineering Task Risk and Rigor, Rev.]]
: [[2 EN]] [[-]]
: [[LI]] [[-102, Corrective Action Process, Rev.]]
: [[13 EN]] [[-]]
: [[LI]] [[-106,]]
: [[NRC]] [[Correspondence, Rev. 4]]
: [[IP]] [[-SMM-LI-123, Coordination of the New York State Public Service Commission Regulatory Requirements, Rev.]]
: [[1 EN]] [[-]]
: [[HU]] [[-101, Human Performance Program, Rev.]]
: [[6 EN]] [[-]]
: [[HU]] [[-102, Human Performance Tools, Rev.]]
: [[5 EN]] [[-]]
: [[HU]] [[-105, Human Performance - Managed Defenses, Rev. 6 3-PT-Q98A, Steam Line Pressure Functional Test - Channel 1, Rev. 4  Condition Reports]]
: [[CR]] [[-]]
: [[IP]] [[2-2008-00389]]
: [[CR]] [[-]]
: [[IP]] [[2-2009-01236]]
: [[CR]] [[-]]
: [[IP]] [[2-2009-01237]]
: [[CR]] [[-]]
: [[IP]] [[2-2009-01239]]
: [[CR]] [[-]]
: [[IP]] [[2-2009-01240]]
: [[CR]] [[-]]
: [[IP]] [[2-2009-01533]]
: [[CR]] [[-]]
: [[IP]] [[2-2009-01924]]
: [[IP]] [[3-]]
: [[LO]] [[-2008-00151]]
: [[IP]] [[3-]]
: [[LO]] [[-2008-00173]]
: [[IP]] [[3-2009-01170]]
: [[IP]] [[3-2009-02494]]
: [[IP]] [[3-2009-01550]]
IP3-2009-01903 IP2-2009-02397
Work Orders 00196415-29  51794754-01  51796053-01  51794751-01  Miscellaneous
: [[IMD]] [[-]]
APL-09-001, 2008-2009 Maintenance Department Performance Improvement Plan
Change Management Notice - Job/Task Focused Coaching and Observation Program
: [[2009 YTD]] [[Human Performance Report 3R15 Human Performance Report  Performance Indicators]]
: [[IPEC]] [[Personnel Error Rate]]
: [[IPEC]] [[Human Performance Cycle Event Rate]]
: [[IPEC]] [[Contact Time (Human Performance)]]
: [[IPEC]] [[Non-Consequential Precursor Error Rate]]
IPEC Coaching Contact Time (Radiation Protection)


Attachment
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ACRONY]] [[]]
: [[MS]] [[]]
: [[ADAMS]] [[Agency Wide Document Management System]]
: [[ALARA]] [[As Low As is Reasonably Achievable]]
: [[AMSAC]] [[]]
: [[ATWS]] [[Mitigation Actuation Circuit ANS  Alert and Notification System]]
: [[ATWS]] [[Anticipated Transient without]]
: [[SCRAM]] [[]]
: [[AOP]] [[s  Abnormal Operating Procedure]]
: [[CAP]] [[Corrective Action Program]]
: [[CB]] [[Control Building]]
: [[CCW]] [[Component Cooling Water]]
: [[CEDE]] [[Cumulative Effective Dose Equivalent]]
: [[CFR]] [[Code of Federal Regulations]]
: [[CR]] [[Condition Report]]
: [[CRDM]] [[Control Rod Drive Mechanism]]
: [[CS]] [[Containment Spray]]
: [[DAW]] [[Dry Active Waste DEC Department of Environmental Conservation]]
: [[DID]] [[Defense In Depth]]
: [[DOT]] [[]]
: [[U.S.]] [[Department of Transportation]]
: [[ECCS]] [[Emergency Core Cooling System]]
: [[ECT]] [[Eddy Current Testing]]
: [[EDG]] [[Emergency Diesel Generator]]
: [[EDO]] [[Executive Director of Operations]]
: [[EOP]] [[s  Emergency Operating Procedures]]
: [[EPRI]] [[Electric Power Research Institute]]
: [[ET]] [[Eddy Current (Inservice Inspection Program nomenclature) FCU  Containment Fan Cooler Unit]]
: [[FSAR]] [[Final Safety Analysis Report]]
: [[FSB]] [[Fuel Storage Building]]
: [[GL]] [[]]
: [[NRC]] [[Generic Letter HRA  High Radiation Area I&C  Instrumentation and Controls]]
: [[IST]] [[Inservice Testing]]
: [[LCO]] [[Limiting Condition for Operation]]
: [[LDE]] [[Lens (Eye) Does Equivalent]]
LHRA  Locked High Radiation Area LER Licensee Event Report
mRem  Millirem
: [[MS]] [[Main Steam]]
: [[MW]] [[Monitoring Well]]
: [[NCV]] [[non-cited violation]]
: [[NEI]] [[Nuclear Energy Institute]]
: [[NIST]] [[National Institute of Science and Technology]]
: [[NRC]] [[Nuclear Regulatory Commission]]
: [[NRR]] [[Office of Nuclear Reactor Regulation]]
: [[ODCM]] [[Offsite Dose Calculation Manual]]
: [[PAB]] [[Primary Auxiliary Building]]
PARS  Publicly Available Records PCP  Process Control Program
PI  Performance Indicator
Attachment
: [[PI&R]] [[Problem Identification and Resolution]]
: [[POP]] [[Plant Operating Procedures]]
: [[PM]] [[Preventive Maintenance]]
: [[PRA]] [[Probabilistic Risk Assessments]]
: [[PWR]] [[Pressurized-Water Reactor]]
: [[QA]] [[Quality Assurance]]
: [[RCA]] [[Radiological Controlled Area]]
: [[RCS]] [[Reactor Coolant System]]
: [[RHR]] [[Residual Heat Removal]]
: [[RMS]] [[Radiation Monitoring Systems RP  Radiation Protection]]
: [[RWP]] [[Radiation Work Permit]]
: [[RWST]] [[Reactor Water Storage Tank]]
: [[SCBA]] [[Self-Contained Breathing Apparatus]]
: [[SDE]] [[Shallow Dose Equivalent]]
: [[SDP]] [[Significance Determination Process]]
: [[SFP]] [[Spent Fuel Pool SG Steam Generator]]
: [[SI]] [[Safety Injection]]
: [[SSC]] [[Structures, Systems, and Components]]
: [[SW]] [[Service Water]]
: [[SWP]] [[Service Water Pump]]
: [[TE]] [[]]
: [[DE]] [[Total Effective Dose Equivalent]]
: [[TI]] [[Temporary Instruction]]
: [[TLD]] [[Thermoluminescent Dosimeter]]
: [[TS]] [[Technical Specifications]]
: [[UFSAR]] [[Updated Final Safety Analysis Report UT  Ultrasonic Testing]]
: [[VC]] [[Vapor Containment]]
: [[VHRA]] [[Very High Radiation Area VT  Visual Inspection (Inservice Inspection Program nomenclature)]]
}}
}}

Latest revision as of 09:54, 14 January 2025

IR 05000247-09-003, on 04/01/2009 - 06/30/2009; Indian Point Nuclear Generating (Indian Point) Unit 2; Event Follow-up
ML092240592
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 08/12/2009
From: Mel Gray
Reactor Projects Branch 2
To: Joseph E Pollock
Entergy Nuclear Operations
Gray M
References
FOIA/PA-2010-0133, FOIA/PA-2011-0021 IR-09-003
Download: ML092240592 (39)


Text

August 12, 2009

SUBJECT:

INDIAN POINT NUCLEAR GENERATING UNIT 2 - NRC INTEGRATED INSPECTION REPORT 05000247/2009003

Dear Mr. Pollock:

On June 30, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Indian Point Nuclear Generating Unit 2. The enclosed integrated inspection report documents the inspection results, which were discussed on July 22, 2009, with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents one self-revealing finding of very low safety significance (Green).

Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of its very low safety significance and because it is entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region 1; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region 1, and the NRC Resident Inspector at Indian Point Nuclear Generating Unit 2. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.

In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room of from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mel Gray, Chief

Projects Branch 2

Division of Reactor Projects

Docket No. 50-247 License No. DPR-26

Enclosure:

Inspection Report No. 05000247/2009003

w/ Attachment: Supplemental Information

cc w/encl:

Senior Vice President, Entergy Nuclear Operations Vice President, Operations, Entergy Nuclear Operations Vice President, Oversight, Entergy Nuclear Operations Senior Manager, Nuclear Safety and Licensing, Entergy Nuclear Operations Senior Vice President and COO, Entergy Nuclear Operations Assistant General Counsel, Entergy Nuclear Operations Manager, Licensing, Entergy Nuclear Operations C. Donaldson, Esquire, Assistant Attorney General, New York Department of Law A. Donahue, Mayor, Village of Buchanan J. G. Testa, Mayor, City of Peekskill R. Albanese, Four County Coordinator S. Lousteau, Treasury Department, Entergy Services, Inc.

Chairman, Standing Committee on Energy, NYS Assembly Chairman, Standing Committee on Environmental Conservation, NYS Assembly Chairman, Committee on Corporations, Authorities, and Commissions M. Slobodien, Director, Emergency Planning P. Eddy, NYS Department of Public Service Assemblywoman Sandra Galef, NYS Assembly T. Seckerson, County Clerk, Westchester County Board of Legislators A. Spano, Westchester County Executive R. Bondi, Putnam County Executive C. Vanderhoef, Rockland County Executive E. A. Diana, Orange County Executive T. Judson, Central NY Citizens Awareness Network M. Elie, Citizens Awareness Network Public Citizen's Critical Mass Energy Project M. Mariotte, Nuclear Information & Resources Service F. Zalcman, Pace Law School, Energy Project L. Puglisi, Supervisor, Town of Cortlandt Congressman John Hall Congresswoman Nita Lowey Senator Kirsten E. Gillibrand Senator Charles Schumer G. Shapiro, Senator Gillibrand 's Staff J. Riccio, Greenpeace P. Musegaas, Riverkeeper, Inc.

M. Kaplowitz, Chairman of County Environment & Health Committee A. Reynolds, Environmental Advocates D. Katz, Executive Director, Citizens Awareness Network K. Coplan, Pace Environmental Litigation Clinic M. Jacobs, IPSEC W. Little, Associate Attorney, NYSDEC M. J. Greene, Clearwater, Inc.

R. Christman, Manager Training and Development J. Spath, New York State Energy Research, SLO Designee F. Murray, President & CEO, New York State Energy Research A. J. Kremer, New York Affordable Reliable Electricity Alliance (NY AREA) ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mel Gray, Chief

Projects Branch 2

Division of Reactor Projects

Docket No. 50-286 License No. DPR-64

Enclosure:

Inspection Report No. 05000286/2009003

w/ Attachment: Supplemental Information

Distribution w/encl:

(via E-mail)

S. Collins, RA M. Dapas, DRA D. Lew, DRP J. Clifford, DRP L. Trocine, RI OEDO R. Nelson, NRR N. Salgado, NRR M. Kowal, NRR J. Boska, PM, NRR J. Hughey, NRR M. Gray, DRP B. Bickett, DRP S. McCarver, DRP P. Cataldo, SRI, IP3 D. Hochmuth, DRP D. Bearde, DRP ROPReportsResources@nrc.gov RI Docket Room (with concurrences

SUNSI Review Complete: __bab___(Reviewers Initial)

DOCUMENT NAME: G:\\DRP\\BRANCH2\\a - Indian Point 2\\Inspection Reports\\IP2 IR2009-003\\IP2 2009.003. r2.doc After declaring this document An Official Agency Record it will be released to the Public To Receive a copy of this document, indicate in the box: C = Copy without attachment/enclosure E = Copy with attachment/enclosure N = No copy

ML0922240592 Office RI/DRP

RI/DRP

RI/DRP

Name GMalone/bab for BBickett/bab MGray/mxg Date 07/31/09 08/05/09 08/12/09

OFFICAL AGENCY RECORD

Enclosure

U.S. Nuclear Regulatory Commission

Region I

Docket No.:

50-247

License No.:

DPR-26

Report No.:

05000247/2009003

Licensee:

Entergy Nuclear Northeast (Entergy)

Facility:

Indian Point Nuclear Generating Unit 2

Location:

450 Broadway, GSB

Buchanan, NY 10511-0249

Dates:

April 1, 2009 through June 30, 2009

Inspectors:

G. Malone, Senior Resident Inspector - Indian Point 2

C. Hott, Resident Inspector - Indian Point 2

D. Johnson, Physical Security Inspector

J. Noggle, Senior Health Physicist

S. McCarver, Project Engineer

E. Huang, Reactor Inspector

O. Ayegbusi, Reactor Inspector

Approved By:

Mel Gray, Chief

Projects Branch 2

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000247/2009003; 04/01/2009 - 06/30/2009; Indian Point Nuclear Generating (Indian Point)

Unit 2; Event Follow-up.

This report covered a three-month period of inspection by resident and region based inspectors.

One finding of very low significance (Green) was identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process. The cross-cutting aspect for the finding was determined using IMC 0305, Operating Reactor Assessment Program. Findings for which the significance determination process (SDP) does not apply may be Green, or be assigned a severity level after NRC management review. The NRCs program for overseeing safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

Cornerstone: Mitigating Systems

Green.

The inspectors documented a self-revealing finding of very low safety significance because Entergy engineers did not provide adequate guidance in a design change package for installation of tubing in the 21 main boiler feedwater pump (MBFP) control system that eventually led to the tubing failure and an unplanned trip of the reactor plant. Entergys design change procedure required that instructions delineating installation precautions be provided in the design change package. Entergys corrective actions included repairing the affected tubing, identifying and replacing similar tubing on the 22 MBFP, and examining Unit 3 MBFPs to identify the extent of the condition. Entergy staff placed this issue into the corrective action program and performed a root cause analysis.

The finding was more than minor because it was associated with the design control attribute of the Initiating Events cornerstone and affected its objective to limit the likelihood of events that affect plant stability and challenge critical safety functions during shutdown, as well as power operations. Specifically, the incorrectly installed MBFP control tubing resulted in a loss of the 21 MBFP and, ultimately, a reactor trip due to low steam generator water level.

The inspectors determined that the finding was of very low safety significance (Green) using the Phase 2 Indian Point Unit 2 risk-informed inspection notebook, in accordance with IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations.

The inspectors determined there was no cross-cutting issue associated with the finding because the performance deficiency did not reflect current licensee performance.

Specifically, the performance deficiency occurred several years ago and was outside the current assessment period, and procedures have since been improved in the design control, work control and vendor control processes that reduced the likelihood of vendors working on equipment without sufficient training or work instructions. (Section 4OA3)

Other Findings

  • A violation of very low safety significance was identified by Entergy staff and has been reviewed by the inspectors. Corrective actions taken or planned by Entergy staff have been entered into Entergy's corrective action program. The violation and corrective action tracking number is listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Indian Point Unit 2 began the inspection period operating at full reactor power (100%). On April 3, 2009, Entergy operators manually shut down Unit 2 because of lowering water levels in the steam generators caused by the trip of a main boiler feed pump. Following investigation and repairs, operators initiated reactor start-up and the plant reached full power operation on April 5, 2009. The reactor trip and associated equipment issues are described further in Section 4OA3. Unit 2 remained at or near full power during the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Summer Readiness of Offsite and Alternate AC Power Systems

a. Inspection Scope

The inspectors verified that plant features and procedures for operation and continued availability of offsite and alternate AC power systems were appropriate. Specifically, the inspectors reviewed station procedures that describe roles, responsibilities, and actions related to the control of switching operations, emergency operations, and degraded conditions on the 13.8kV, 138kV, and 345kV electric power distribution system in the Buchanan Switchyard and onsite at Indian Point. Additionally, the inspectors walked down portions of the Buchanan Switchyard, onsite high voltage components, and the Appendix R diesel generator. The inspectors reviewed outstanding maintenance work orders and condition reports (CRs) related to these systems to verify Entergy personnel were appropriately prioritizing work and correcting problems in accordance with station procedures. Documents reviewed are listed in the Attachment.

b. Findings

No findings of significance were identified.

.2 Station Readiness for Summer Heat Conditions

a. Inspection Scope

The inspectors reviewed the readiness of risk-significant systems for summer hot weather conditions. The inspectors reviewed Entergys adverse weather procedures, operating experience, corrective action program, Updated Final Safety Analysis Report (UFSAR),

Technical Specifications (TS), operating procedures, staffing, and applicable plant documents to determine the types of adverse weather challenges to which the site is susceptible. The inspectors also checked local area temperatures, as well as the operability of ventilation and air conditioning cooling systems, to ensure the plant was prepared for warm weather conditions. In addition, the following risk-significant systems that were required to be protected from adverse weather conditions were selected and collectively represented one inspection sample:

  • 480-Volt system; and

b. Findings

No findings of significance were identified.

.3 Emergent Heat Conditions on April 27-28, 2009

a. Inspection Scope

The inspectors evaluated implementation of the adverse weather preparation procedures and compensatory measures before the onset of, and during adverse weather conditions.

Specifically, the inspectors evaluated Entergys preparations and compensatory measures taken during a period of hot weather from April 27 to April 28, 2009. The inspectors conducted walkdowns of plant equipment and reviewed operating procedures to ensure that equipment important to safety would not be adversely affected by severe weather conditions.

The documents reviewed during this inspection are listed in the Attachment. This inspection satisfied one inspection sample for the onset of adverse weather.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns to verify the operability of redundant or diverse trains and components during periods of system train unavailability or following periods of maintenance. The inspectors referenced system procedures, UFSAR, and system drawings to verify the alignment of the available train supported its required safety functions. The inspectors also reviewed applicable CRs and work orders to ensure Entergy personnel identified and properly addressed equipment discrepancies that could potentially impair the capability of the available train, as required by Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action. The documents reviewed during these inspections are listed in the Attachment.

The inspectors performed a partial walkdown on the following systems, which represented three inspection samples:

  • 21 and 23 component cooling water pumps during maintenance on the 22 component cooling water pump;
  • 21 charging pump during repairs to the 23 charging pump.

b. Findings

No findings of significance were identified.

.2 Full System Walkdown

a. Inspection Scope

The inspectors performed a complete system walkdown of accessible portions of the non-essential service water system to identify discrepancies between the existing equipment lineup and the required lineup. The inspectors reviewed operating procedures, surveillance tests, piping and instrumentation drawings, equipment lineup check-off lists, and the UFSAR to verify the system was aligned to perform its required safety functions. The inspectors reviewed a sample of CRs written to address deficiencies associated with the system to ensure they were appropriately evaluated and resolved. The documents reviewed during this inspection are listed in the Attachment. The walkdown of the non-essential service water system represented one inspection sample.

b. Findings

No findings of significance were identified.

==1R05 Fire Protection

==

.1 Resident Inspector Quarterly Walkdowns

a. Inspection Scope

The inspectors conducted tours of several fire areas to assess the material condition and operational status of fire protection features. The inspectors verified, consistent with the applicable administrative procedures, that: combustibles and ignition sources were adequately controlled; passive fire barriers, manual fire-fighting equipment, and suppression and detection equipment were appropriately maintained; and compensatory measures for out-of-service, degraded, or inoperable fire protection equipment were implemented in accordance with Entergys fire protection program. The inspectors evaluated the fire protection program for conformance with the requirements of License Condition 2.K. The documents reviewed during this inspection are listed in the Attachment. This inspection represented seven inspection samples for fire protection tours, and was conducted in the following areas:

  • Fire Zone 5, 21 charging pump room;
  • Fire Zone 6, 22 charging pump room;
  • Fire Zone 7, 23 charging pump room;
  • Fire Zone 1, component cooling pump room;
  • Fire Zone 11, cable spreading room; and

b. Findings

No findings of significance were identified.

.2 Annual Fire Drill Sample

a. Inspection Scope

The inspectors observed the fire brigades response to an actual fire alarm on May 18, 2009.

The fire brigade was dispatched to a manhole inside the protected area containing 138kV offsite power cables used to allow power to be cross-connected between Unit 2 and Unit 3 138kV switchyards. The inspectors verified the fire brigade responded to the call in a timely manner, protective clothing and turnout gear was properly worn, appropriate fire fighting equipment was selected and made ready for use, and the fire brigade leader exhibited command-and-control of the scene.

b. Findings

No findings of significance were identified. The heat and smoke identified in the manhole were due to an electrical fault in the three-phase non-safety related power cables in the vault. Protection relays in the electrical system automatically isolated the fault from the rest of the 138kV switchyard following the fault. There was no other equipment in the manhole and no extinguishing material was required to be discharged.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors completed one internal flood protection sample. The inspectors reviewed selected risk-important plant design features and Entergy procedures intended to protect the plant and its safety-related equipment from internal flooding events. The inspectors focused on mitigation strategies and equipment for the 15 elevation of the auxiliary feed pump building, including the 21, 22, and 23 auxiliary boiler feed pump areas. The inspectors reviewed flood analysis and design documents, including the UFSAR, engineering calculations, and abnormal operating procedures. The inspectors observed the condition of wall penetrations, watertight doors, flood alarm switches, and drains to assess their readiness to contain flow from an internal flood in accordance with the design basis.

b. Findings

No findings of significance were identified.

==1R11 Licensed Operator Requalification Program

==

.1 Quarterly Review

a. Inspection Scope

On June 10, 2009, the inspectors observed licensed operator simulator training, which included an anticipated transient without a scram and a loss of primary coolant scenario, to verify operator performance was adequate and evaluators were identifying and documenting crew performance problems. The inspectors evaluated the performance of risk-significant operator actions including the use of emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms, performance of timely control board operation and manipulation, and the oversight and direction provided by the control room supervisor. The inspectors also assessed simulator fidelity with respect to the actual plant. The inspectors evaluated licensed operator training for conformance with the requirements of 10 CFR Part 55, Operator Licenses. The documents reviewed during this inspection are listed in the

. This observation of operator simulator training represented one inspection sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed performance-based problems that involved structures, systems, and components (SSCs) to assess the effectiveness of maintenance activities.

When applicable, the reviews focused on:

  • Proper maintenance rule scoping in accordance with 10 CFR 50.65;
  • Characterization of reliability issues;
  • Changing system and component unavailability;
  • Identifying and addressing common cause failures;
  • Trending of system flow and temperature values;
  • Appropriateness of performance criteria for SSCs classified (a)(2); and
  • Adequacy of goals and corrective actions for SSCs classified (a)(1).

The inspectors also reviewed system health reports, maintenance backlogs, and maintenance rule basis documents. The inspectors evaluated maintenance effectiveness and monitoring activities against the requirements of 10 CFR 50.65. The documents reviewed during this inspection are listed in the Attachment. The following samples were reviewed and represented two inspection samples:

  • Primary water make-up system; and

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed scheduled and emergent maintenance activities to verify that the appropriate risk assessments were performed prior to removing equipment from service for maintenance or repair. The inspectors reviewed selected risk assessments to verify assessments were performed as required by 10 CFR 50.65(a)(4), and were accurate and complete. When emergent work was performed, the inspectors reviewed the plant risk to ensure risk was promptly reassessed and managed. Documents reviewed during this inspection are listed in the Attachment. The following activities represented nine inspection samples:

  • Planned maintenance on 22 auxiliary boiler feed pump during undervoltage relay replacement;
  • Planned maintenance on 96951 138kV feeder line during 21 safety injection pump and valve testing;
  • Planned maintenance on 21 primary water pump, 22 service water pump, 22 component cooling water pump, and the 96952 138kV feeder line;
  • Planned maintenance activities during the week the 138kV cross-tie feeder line 33332 experienced a fault to ground and remained out of service;
  • Emergent work on 22 circulating water pump and 23 containment fan coil unit with the 138kV cross-tie feeder line 33332, 21 primary water pump and valve FCV-110A out of service for maintenance;
  • Emergent work activities associated with the 345kV breakers 7 and 11 (line 95891)with the 138kV line 33332 and 21 primary water pump out of service; and
  • Emergent work activities associated with the 23 charging pump, 22 stator water cooling pump, and trip of the 23 motor control center.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

.1 Resident Quarterly Review

a. Inspection Scope

The inspectors reviewed operability evaluations to assess the acceptability of the evaluations, the use and control of compensatory measures when applicable, and compliance with Technical Specifications (TS). The inspectors reviews included verification that operability determinations were performed in accordance with procedure ENN-OP-104, Operability Determinations. The inspectors assessed the technical adequacy of the evaluations to ensure consistency with the TS, UFSAR, and associated design basis documents (DBDs). The documents reviewed are listed in the Attachment.

The following operability evaluations were reviewed and represented seven inspection

samples:

  • 22 auxiliary boiler feed pump (ABFP) bearing conditions;
  • 22 ABFP steam admission valve leak-by (PCV-1139);
  • Seismic qualification of vital 480V manholes;
  • Seismic qualification of service water piping located at the intake structure (missing pipe support); and

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

.1 Temporary Modifications

a. Inspection Scope

The inspectors reviewed three conditions as temporary plant modifications. The inspectors reviewed Entergys temporary modification procedure to verify that modifications were processed adequately. The inspectors verified the design bases, licensing bases, and performance capability of the system was not degraded by the temporary modification. In addition, the inspectors interviewed plant staff and reviewed issues entered into the corrective action program to determine whether Entergy had been effective in identifying and resolving problems associated with the temporary modifications. The documents reviewed are listed in the Attachment. The review of these temporary modifications represented three inspection samples. The following modifications were reviewed:

  • Diagnostic equipment stationed external to 21 and 22 static inverters to troubleshoot intermittent inverter alarms and power supply swaps;
  • Diagnostic equipment attached to a control room panel to troubleshoot intermittent grounds on the 21 battery charger; and
  • 21 reactor coolant pump oil fill connection to allow remote filling of bearing reservoirs due to leakage.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance test procedures and associated testing activities for selected risk-significant mitigating systems, and assessed whether the effect of maintenance on plant systems was adequately addressed by control room and

engineering personnel. The inspectors verified that: test acceptance criteria were clear and the test demonstrated operational readiness consistent with design basis documentation; test instrumentation had current calibrations with the appropriate range and accuracy for the application; and the tests were performed as written, with applicable prerequisites satisfied.

Upon completion of the tests, the inspectors reviewed whether equipment was returned to the proper alignment necessary to perform its safety function. Post-maintenance testing was evaluated against the requirements of 10 CFR 50, Appendix B, Criterion XI, Test Control.

The documents reviewed are listed in the Attachment. The following post-maintenance activities were reviewed and represented three inspection samples:

  • Calibration and replacement of undervoltage relays 27-52 and 27-53 on bus 5A; and
  • Post-maintenance test associated with the 2-year overhaul of the 28 service water traveling water screen.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed performance of portions of surveillance tests and/or reviewed test data for selected risk-significant SSCs to assess whether tests satisfied TS, UFSAR, Technical Requirements Manual, and Entergy procedure requirements. The inspectors verified that: test acceptance criteria were clear, demonstrated operational readiness, and were consistent with design basis documentation; test instrumentation had accurate calibration, and appropriate range and accuracy for the application; and tests were performed as written, with applicable prerequisites satisfied. Following the tests, the inspectors verified that the equipment was capable of performing the required safety functions. The inspectors evaluated the surveillance tests against the requirements in TS.

The documents reviewed during this inspection are listed in the Attachment. The following surveillance tests were reviewed and represented five inspection samples:

  • 2-PT-Q38, primary water storage tank level;
  • 2-PT-M108, safety injection system venting;
  • 2-PT-Q030C, 23 component cooling water pump in-service test;
  • 2-PT-Q59, containment pressure bistables; and
  • 2-PT-Q029B, 22 safety injection pump.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Public Radiation Safety (PS)

2PS2 Radioactive Materials Processing and Shipping (71122.02 - 6 samples)

a. Inspection Scope

From June 22 to June 26, 2009, the inspectors conducted the following activities to verify that Entegy=s radioactive material processing and transportation programs complied with the requirements of 10 CFR 20, 61, and 71; and Department of Transportation (DOT) regulations 49 CFR 170-189.

(1) The inspectors reviewed the solid radioactive waste system description in the UFSAR, the 2008 radiological effluent release report for information on the types and amounts of radioactive waste disposed, and the scope of the licensee=s audit program to verify that it meets the requirements of 10 CFR 20.1101.
(2) The inspectors walked-down the liquid and solid radioactive waste processing systems to verify and assess that the current system configuration and operation agree with the descriptions contained in the UFSAR and in the Process Control Program (PCP); and reviewed the status of radioactive waste process equipment that is not operational and/or is abandoned in place; verified changes were reviewed and documented in accordance with 10 CFR 50.59, as appropriate. The inspectors reviewed the current processes for transferring and dewatering of radioactive waste resin and sludge discharges into shipping/disposal containers to determine if appropriate waste stream mixing and/or sampling procedures, and methodology for waste concentration averaging provide representative samples of the waste product for the purposes of waste classification as specified in 10CFR 61.55 for waste disposal.
(3) The inspectors reviewed the radio-chemical sample analysis results for the licensee=s radioactive waste streams, reviewed the licensee=s use of scaling factors and calculations with respect to these radioactive waste streams to account for difficult-to-measure radionuclides, verified the licensee=s program assures compliance with 10 CFR 61.55 and 10 CFR 61.56 as required by Appendix G of 10 CFR 20, and reviewed Entergys program to ensure the waste stream composition data accounts for changing operational parameters and thus remains valid between the annual or biennial sample analysis update.
(4) From June 24 to June 25, 2009, Entergy personnel prepared, packaged, and completed shipment No.09-109 containing spent filters in a Type A cask for shipment to a waste processor. The inspectors observed the shipment preparations that included: packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifests, shipping papers provided to the driver, and licensee verification of shipment readiness.
(5) The inspectors sampled the following non-excepted package shipment records and reviewed these records for compliance with NRC and DOT requirements:

$

08-055, spent fuel pool demineralizers shipment to a waste processor on April 7, 2008;

$

08-093, Hudson River silt shipment to a waste processor on May 15, 2008;

$

08-170, sodium hydroxide shipment to a waste processor on September 4, 2008;

$

08-200, Unit 1 debris shipment to a waste processor on November 4, 2008;

$

08-223, fuel sipping equipment shipment to Westinghouse on December 15, 2008;

$

09-068, dry active waste shipment to a waste processor on April 15, 2009;

$

09-100, Unit 1 pool sludge shipment to a waste processor on June 10, 2009;

$

09-102, Unit 2 primary resin shipment to a waste processor on June 17, 2009;

$

09-103, Unit 3 bead resin shipment to a waste processor on June 17, 2009; and

$

09-109, spent filter shipment to a waste processor on June 25, 2009.

(6) The inspectors reviewed Entergy=s Licensee Event Reports, Special Reports, audits, State agency reports, and self-assessments for Indian Point Unit 2 related to the radioactive material and transportation programs performed since the last inspection to determine if identified problems are entered into the corrective action program for resolution. The inspectors also reviewed corrective action reports written against the radioactive material and shipping programs since the previous inspection.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed performance indicator data for the cornerstones listed below and used Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, to verify individual performance indicator accuracy and completeness. The documents reviewed during this inspection are listed in the Attachment.

Initiating Events Cornerstone

  • Unplanned Scrams with Complications

Mitigating Systems Cornerstone

  • Safety System Functional Failures; and

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of all items entered into Entergys corrective action program. The review was accomplished by accessing Entergys computerized database for CRs and attending condition report group screening meetings.

In accordance with the baseline inspection modules, the inspectors selected corrective action program items across the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for further follow-up and review. The inspectors assessed Entergy personnels threshold for problem identification, adequacy of the causal analysis, extent of condition reviews, and operability determinations, and timeliness of the associated corrective actions.

b. Findings

No findings of significance were identified.

.2 Annual Sample: Review of Corrective Actions Related to the Installation and Project

Management of the New Alert and Notification System (ANS) (71152 - 1 sample)

a. Inspection Scope

The inspectors reviewed Entergy staff=s actions in response to CRs generated as a result of issues associated with the installation and project management of the new alert and notification system (ANS) for the Indian Point Energy Center. The inspectors reviewed Entergy procedures on project management and external stakeholder communications. In addition, the inspectors interviewed applicable members of Entergys staff including a lead project manager and licensing staff. The focus of this inspection was to verify that the corrective actions, reviewed during the December 2008 Enforcement Follow-up Inspection (Inspection Procedure 92702, NRC Inspection Report 50-247/286, 2008-503, dated January 27, 2009), were being completed in a thorough and timely manner.

b. Findings

& Observations

No findings of significance were identified. The inspectors reviewed CRs documenting issues related to the installation and project management of the new ANS placed into service for the Indian Point Energy Center in 2008. The inspectors determined Entergy personnel implemented or generated plans for appropriate corrective actions to address each issue that was identified. Additionally, the inspectors verified that Entergy staff appropriately implemented or generated plans for corrective actions to revise the project management process, require greater senior management oversight for projects, and develop a new procedure for interactions with external stakeholders.

.3 Annual Sample: Station Auxiliary Transformer Tap Changer Alarms

a. Inspection Scope

The inspectors reviewed Entergy staffs evaluations and corrective actions associated with the station auxiliary transformer tap changer hang-up alarms. Entergy staffs evaluations determined that for the tap changer alarm to occur: the tap changer is either in-between taps and a time delay of 12 seconds has passed; or the tap changer is greater than or equal to 16 taps in the raise or lower direction and a time delay of 12 seconds has passed. The alarm could also occur if there is a problem with the alarm circuitry. The inspectors reviewed Entergy staffs corrective actions to ensure that appropriate evaluations were performed and corrective actions were specified and prioritized. The inspectors also reviewed the follow-up actions to verify that the corrective actions identified were implemented.

b. Findings

& Observations

No findings of significance were identified.

The inspectors determined Entergys corrective action associated with the station auxiliary transformer tap changer hang-up alarms was appropriate. Entergys corrective actions in 2007 were to examine the alarm circuitry in addition to the scheduled preventive maintenance in the refueling outage of 2008. The inspectors noted that the 2008 preventive maintenance that was performed provided satisfactory results; however, the alarm issue continued to occur following the outage. Entergy personnel currently respond to the alarms by entering the appropriate alarm response procedure and TS 3.8.1 action statement each time the alarm occurs as well as manually verifying that the tap changer remained functional.

Entergy personnel are currently tracking and trending the alarms and plan to adjust the cam rollers of the tap changer in the spring outage of 2010. From the data of the last two alarms, Entergy staff indicated the two cam switches that communicate between the alarm circuit and the motor are not synchronized and an adjustment of the cam rollers should resolve the alarms. The inspectors determined that previous surveillance tests demonstrated the alarm circuitry is operable and the alarm will actuate on a valid signal. The inspectors determined the alarms appear to be an alarm issue only not an actual tap changer performance problem at this time. The inspectors determined the tap changer is able to perform its required function and corrective actions in place by Entergy personnel are adequate and commensurate with the risk significance of the issue.

.4 Annual Sample: Review of Service Water Pump Motor Termination Failure (71152 - 1

sample)

a. Inspection Scope

The inspectors selected CR-IP2-2008-00414 as a problem identification and resolution (PI&R) sample for a detailed follow-up review. CR-IP2-2008-00414 documented a failure of the 21 service water pump (SWP) motor B phase termination that resulted in the pump being declared inoperable on January 24, 2008. Entergy personnel determined the failure was due to the installation of an undersized cable termination lug during the previous replacement of the 21 SWP motor in April 2005. The inspectors assessed Entergy staffs problem identification threshold, apparent cause evaluation, extent of condition review, and the prioritization and timeliness of corrective actions to determine whether personnel were appropriately identifying, characterizing, and correcting problems associated with this issue and whether the planned or completed corrective actions were appropriate.

b. Findings and Observations

No findings of significance were identified.

The inspectors determined Entergy personnel adequately implemented its corrective action process regarding the initial discovery of the above issue. The CR packages were complete and included an apparent cause evaluation, extent of condition reviews, completed and planned corrective actions. Additionally, the elements of the CR packages were detailed and thorough. Specifically, the inspectors noted Entergy personnel implemented a new procedure for installing electric motor terminations EN-425-TER, Installation of Electric Motor Terminations. Also, Entergy trainers provided refresher training on performing electric motor terminations to the maintenance department and revised the electricians lesson plan EMF-EWS-01, Electrical Workmanship Standards to include training on electric motor terminations and scheduled the installation of infrared windows on the motor termination box for periodic thermography inspections. In addition, Entergy personnel revised 2-PMP-004-SWS, IP2 Service Water Pump and Motor Replacement Procedure, to use EN-425-TER for installing electrical motor terminations. As part of the extent of condition, Entergy staff performed detailed visual and thermography inspections of a selection of motor terminations. The inspectors determined the anomalies found during those inspections were adequately addressed.

During the inspection, the inspectors noted that the new procedure, EN-425-TER, was in a reserved status and the CR was closed indicating all corrective actions were completed.

Entergy staff overlooked activating EN-425-TER because 2-PMP-004-SWS had not been revised to reference the new procedure for installing electric motor terminations. The inspectors determined the issue was of minor significance because ENN-EE-S-008-IP had been revised to perform the same function as EN-425-TER and was available for use.

Following discussions with the inspectors, Entergy staff activated EN-425-TER and revised 2-PMP-004-SWS accordingly. The inspectors determined the corrective actions were timely and appeared appropriate to resolve the above issue. The inspectors determined these corrective actions addressed immediate equipment concerns as well as the extent of condition of the problem. In addition, the inspectors determined that adequate tracking mechanisms were in place to ensure scheduled corrective actions should be completed.

.5 Annual Sample: Review of Root Cause Analysis and Actions Addressing the Underground

Pipe Leak to the Condensate Storage Tank Return Line (71152 - 1 sample)

a. Inspection Scope

The inspectors reviewed Entergy staffs root cause analysis (RCA) for a leak in a section of underground return piping to the condensate storage tank (CST) that was identified on February 15, 2009. The inspectors reviewed the report and pertinent documents and interviewed station personnel to determine if the RCA adequately identified the causes of the leak, considered the extent of the problem, and provided for adequate corrective actions.

Background

On February 15, 2009, at approximately 3:00 p.m., an operator on rounds observed water in the CST return pipe sleeve where the pipe enters the auxiliary feed pump building floor.

Entergy staff took chemistry samples of the water and subsequently determined that 54 parts per billion (ppb) hydrazine was present, indicating that the water was likely from the condensate system. At 1:30 a.m. on February 16, operators declared the CST inoperable.

By February 18, Entergy staff determined the leak rate from the CST was approximately 17 gallons per minute (gpm), commenced excavation of the probable leak location, and confirmed that the leakage was from the CST return piping. On February 19, the excavation of the CST piping exposed the leak on the CST return pipe. Entergy technicians removed the pipe coating from the surrounding areas and performed ultrasonic testing of the pipe walls and determined the removed pipe was structurally sound and the metal loss was localized to the area of the pipe coating degradation. In addition to the hole identified in the horizontal run of the return pipe, Entergy staff discovered areas of minor metal loss on a pipe elbow in the same line due to pipe coating degradation. Entergy personnel removed the damaged section of piping and elbow and welded a new pipe portion in place on February 20. The CST was declared operable at 6:56 a.m. on February 21.

Entergy staff performed a RCA to determine the causes of the CST pipe leak. Entergy staff also contracted a vendor to analyze the portion of piping that was removed to determine the failure mode mechanisms. During excavation, Entergy staff identified a portion of the pipe backfill contained rocks ranging in size from 3 to 8 inches. Entergy staff reviewed the backfill specifications used during plant construction and determined the specifications did not provide detailed information on what size rocks could be present in this area. Entergy staff determined this particular area had a concrete slab poured on top of the fill and the slab was not intended to be a load bearing surface and, therefore, was not specific in requirements for the type of fill to be used. The vendor analysis of the pipe concluded that the leak was caused by external corrosion in areas where the pipe coating was degraded. Although the exact type of external corrosion could not be definitively concluded, Entergy staff determined the corrosion was likely the result of exposure to a range of ground water characteristics, and/or microbiologically influenced corrosion. Entergys RCA documented that the large rocks found in the backfill likely damaged the pipe coating during installation of the pipe and allowed the corrosion mechanisms described above to act on the localized metal surfaces.

Entergy staff determined the pipes were found to be in good condition where the coating was intact.

Entergys root cause team examined the stations capability to track water usage to determine whether it was reasonable for staff to identify the leakage prior to February 15.

The root cause team determined that it was not feasible for operators to detect the leakage from main condenser hotwell level indications or CST level indications because the rate of leakage (10-17gpm) was too small to detect considering the tank volumes and installed instrumentation. Furthermore, the root cause team supported its conclusion because several sources contribute to normal losses of inventory in the hotwell and require replenishment from the CST such as steam generator blowdown, non-safety auxiliary steam heating, and typical leakage from the non-safety related condensate system. Additionally, control room operators periodically monitor the decrease in CST level and make-up to the CST as necessary to ensure the CST level is maintained within required limits.

Entergys root cause team developed a corrective action plan to address the root and contributing causes of the pipe degradation. As part of those corrective actions, Entergy staff identified additional buried pipe inspections at several locations based on similar corrosion susceptibilities. Specifically, the root cause documentation described the Indian Point Buried Piping and Tank Inspection Program that has been under development since 2007, as part of a corporate-wide initiative to develop these programs at all Entergy sites.

The program identifies underground pipes at the site and assigns an impact assessment level based on safety impact of a failure. The high impact systems are also corrosion risk assessed by considering soil conditions, pipe material, and existing coatings or cathodic protection. The scheduling of examination of the pipes is determined by the potential safety impact and corrosion risk assessments. The non-destructive examinations may involve the use of guided wave technology, excavation and visual inspection, or other appropriate techniques as determined by Entergy personnel. Entergy managers plan to have the buried piping program fully developed by the end of 2009.

Entergys corrective action plan included the following actions listed below:

  • Update the buried piping backfill and excavation specification;
  • Implement improved inspection techniques for buried piping;
  • Evaluate the need for cathodic protection systems and draining systems for select buried piping;
  • Evaluate the use of existing monitoring wells for buried pipe and tank leaks for early detection capability;

o CST return line (2 different locations)o CST supply line (2 different locations)o Service water line 408 (2 different locations); and

  • Remainder of underground piping to be inspected in accordance with Buried Piping Program schedule.

As further background, by letter dated July 27, 2009, as clarified by letter dated August 6, 2009, Entergy management submitted an amendment to their license renewal application which modified the Indian Point Buried Piping and Tanks Inspection Program. This amendment reflected Entergys operating experience with the CST buried pipe leak at Unit 2 and included identification of additional buried pipe examinations. These non-destructive examinations will be performed by Entergy personnel at Units 2 and 3 prior to entering the period of extended operation and will supplement the six additional inspections referenced above.

b. Findings and Observations

No findings of significance were identified.

Overall, the inspectors reviewed Entergy staff activities related to the CST return line leak and the associated RCA and determined that Entergys staff identified the likely causes of the leak, considered the extent of the problem, and planned or provided for adequate corrective actions. Additionally, the inspectors concluded that Entergys root cause team adequately considered prior opportunities for identifying the CST return line leak.

The inspectors independently reviewed plant drawings and the backfill specifications provided by the engineer/architect at the time of plant construction and determined the drawings and specification did not detail or place limits on the type of backfill required and specifically did not prohibit rocks from being used in the backfill.

The inspectors noted that Entergy personnel performed required testing in accordance with the American Society of Mechanical Engineers Boiler & Pressure Vessel (ASME BPV) Code Section XI and 10 CFR 50.55a. ASME Section XI requires pipes similar to the CST return line be tested three times over the 10-year inspection interval by a pressure drop or flow test.

The inspectors determined that Entergy had procedures in place to implement ASME Code requirements for testing the subject CST retun line piping.

The inspectors considered whether the RCA evaluated the potential for Entergy personnel to identify the pipe leak prior to February 15, 2009. The inspectors concluded that Entergys RCA adequately considered prior opportunities for Entergy staff to identify the leak and that Entergy staff identified the leak when reasonable to do so. However, the inspectors identified two examples in which the RCA did not consider corrective actions that might aid Entergy staff in the early identification of leaks in the future should they occur.

  • Entergys RCA evaluated Unit 2 CST level losses and condensate flow paths prior to February 2009 with a focus on the operators ability to identify secondary level changes that would be indicative of a CST leak. The root cause team concluded it would not be reasonable for operators to identify a secondary leak of 10-20 gpm on the Unit 2 CST using the installed instrumentation because the leak was very small compared to the large volume of the CST. While the RCA considered the CST volume and water usage flow paths, the inspectors determined the RCA did not consider or document an evaluation with respect to existing daily operational logs that could provide trend information on overall processed monthly water usage and make-up to the Unit 1 CST.

The inspectors review identified that operations personnel log the processed water sent from the stations on-site city water system to the Unit 1 CST such that the amount of water used daily by secondary plant operations on Unit 2 can be trended. The inspectors review of water usage identified a noticeable increase in water consumed by Unit 2 in November 2008 with a continued increase through February 2009 compared to typical water usage in prior years during the same months. When interviewed by inspectors, Entergy staff explained the log reading is used to verify station billing from the water conditioning vendor and not intended to be trended and tracked for purposes of Unit 2 CST water usage.

The inspectors determined it was not reasonable for Entergy staff to have identified the CST return pipe leak based on the increased water usage as logged for billing purposes considering there was not a prior history of CST pipe leaks. However, the inspectors review determined Entergys RCA did not document its evaluation of the capability to trend logged water usage data from year to year. Additionally, Entergys RCA did not evaluate whether this water usage data could be useful, in concert with other monitoring activities, to identify indications of potential leaks in the future as early as reasonably possible, whether they occur from safety related or non-safety related components.

  • Entergys RCA reviewed previous inspection results for excavation of two sections of CST piping that were conducted by Entergy staff in October and November 2008 in response to recommendations from an Independent Safety Evaluation Report dated July 31, 2008. The excavated areas were located in areas between the CST and the auxiliary feed pump building. At that time, Entergy staff identified, based on non-destructive examinations, five areas of piping that required coating repair due to missing or damaged pipe coating. The inspectors review of Entergys examinations noted that the pipe walls at those locations in 2008 remained at or near their original manufactured thickness.

Based on observations and repairs made, Entergys staff concluded the pipes did not exhibit pipe degradation that would warrant further inspection of these same locations in the future. Additionally, the inspectors noted Entergys RCA described that during the 2008 excavations, Entergy staff observed water visible in a CST return line pipe collar where the piping entered the auxiliary feed pump building. Entergy staff performed chemistry analysis of this water and concluded, based on the sample results, that the pH, tritium levels, and absence of hydrazine indicated the leakage was consistent with groundwater chemistry during a time of heavy rains and was not indicative of CST water chemistry.

The inspectors concluded Entergy staff adequately assessed conditions surrounding the 2008 excavations. However, the inspectors determined the RCA did not evaluate the water present in the CST return pipe collar in October 2008 specific to the issue not being entered into the corrective action program. The inspectors determined it would have been appropriate for the RCA to evaluate whether corrective actions were appropriate to reinforce the expectations for staff to enter unanticipated visual indications of water in the CST pipe return floor collar within the corrective action program to provide awareness to senior managers and provide an opportunity to trend the condition. The inspectors concluded this issue was a performance deficiency of minor significance based on the actions taken by Entergy staff at that time which included chemistry results that supported Entergys assessment the water was not indicative of CST water chemistry and tritium levels were well below regulatory limits for release to the environment.

.6 Semi-Annual Trend Review

a. Inspection Scope

In July 2009, inspectors reviewed Entergy staffs progress in implementing corrective actions identified in 2008 to address Human Performance issues as outlined in Entergys Human Performance Improvement Plan with a focus on specific efforts since January 2009. The inspectors evaluated staff performance improvement plans and actions using inspection guidance in Inspection Procedure 71152, Identification and Resolution of Problems.

Specifically, the inspectors assessed Entergys progress in addressing human performance by evaluating whether Entergys internal milestones were being monitored and consistently met and whether adjustments in approach were made when necessary. This inspection focused on the actions implemented since January 2009.

The inspectors conducted a review of the applicable condition reports (CRs), corrective action assignments (CAs), focused self-assessments, Quality Assurance group assessments, and causal evaluations for human performance events and errors. The inspectors also reviewed Entergy internal performance indicators related to their performance improvement plan, and reviewed a sample of revised procedures in order to assess the adequacy of the performance plan and effectiveness of corrective actions.

b. Findings and Observations

No findings of significance were identified.

In late December 2008, NRC inspectors independently reviewed the causal evaluation and corrective actions focused on an emerging trend, identified by Entergy, and associated with human performance errors. Entergy staff and managers identified several events, attributable to human performance errors that occurred at Indian Point (both units) in 2008, which resulted in personal injury and/or equipment failures. The inspectors determined that Entergy managers recognized this adverse trend in human performance, and developed a Human Performance Program to address the causes of the events, and to assist in the prevention or mitigation of future occurrences. The inspectors noted that the Human Performance Program included actions to understand the causes of human performance errors, to reduce these human performance errors in the future, and to monitor future performance.

The inspectors determined Entergy staff and managers developed station-wide communication tools, training plans, and adjusted the site business plan to address these common causes of human performance errors. New communication tools developed included Safety and Human Performance Stand Downs and periodic human performance bulletins. The Safety and Human Performance Stand Downs were used to develop a forum to reinforce site human performance expectations and discuss recent human performance error events. Entergy managers also scheduled future stand downs to coincide with major evolutions on site in 2009, such as the Unit 3 refueling outage.

The inspectors noted that Entergy staff developed a Human Performance Simulator and Work Management Academy to provide training on human performance traps, human performance tools, and to improve work planning and execution. The Human Performance Simulator focuses on reinforcing the proper threshold for identifying error traps and the effective use human performance tools to accomplish tasks. Operations and maintenance departments have completed this training, and it will now be included as annual refresher training for their department personnel. The Work Management Academy was required for all supervisory personnel and reinforced Entergys work management model and procedures. Entergy staff and managers also developed its Thought Improvement Process (TIP) Initiative to encourage employees to provide constructive feedback to improve the sites human performance.

The inspectors also noted that Entergy staff and managers established commitments to monitor future human performance at Indian Point. In particular, human performance indicators and self-assessment results would be used to monitor the effectiveness of the current programs and for evaluation of future trends in human performance. The inspectors concluded that Entergy took action to address the sites emerging adverse human performance trend. The programs established within Entergys Human Performance program were determined to be reasonable to address the recent human performance.

During the July 2009 semi-annual trend review, inspectors determined that Entergy staff continued to make progress in implementing their corrective action plans to address human performance issues related to error prevention and to make adjustments to those actions based on the results of self-assessments, performance indicators, and benchmarking. For example, based on observations of supplemental workers during the recent Unit 3 refueling outage, actions were being developed to provide additional oversight of supplemental workers. The inspectors also noted that, in accordance with previous corrective actions, Entergy staff and managers had:

  • Continued to use the Human Performance Simulator to train various departments, and to check and adjust development of dynamic learning activities in the simulator;
  • Implemented a standard schedule for site wide stand downs during outage and non-outage periods;
  • Revised pre-job briefing procedures to include signature accountability,
  • Implemented a task/job observation program aligned with the work control process and Most Error Likely Task-focused crew assessments;
  • Assigned experienced mechanics, technicians, and operators to procedure groups;
  • Reinforced critical procedure steps through the use of special markings, briefs, and feedback;
  • Filled key personnel vacancies previously identified as necessary to strengthen the organizations effectiveness in preventing human error;
  • Improved adherence to online and outage work management milestones;
  • Improved effectiveness of work package walk downs and feedback;
  • Established weekly work package quality meetings.

Additionally, the inspectors noted that Entergy has developed additional performance indicators to assist in monitoring progress in addressing human errors, and is planning to conduct annual Human Performance training to first-line supervisors and above.

The recent trend in human performance related to error prevention indicated that corrective actions, to date, have not resulted in a decrease in the human error rate trend, primarily due to issues that occurred during the Unit 3 refueling outage. Notwithstanding, the inspectors concluded that station management has adjusted its actions/focus as a result of its evaluation of additional performance information, especially from the outage. The programs and actions established within Entergys Human Performance program were determined to be reasonable to address the recent human performance issues related to error prevention.

4OA3 Event Follow-Up

.1 Reactor Trip on April 3, 2009, Due to Low Steam Generator Water Levels

a. Inspection Scope

The inspectors responded to the control room on April 3, 2009, following a manual insertion of all control rods (manual reactor trip) by control room operators due to lowering water levels in all four steam generators (SGs) due to a combination of an unexpected 21 main boiler feed pump (MBFP) shutdown and failure of the main turbine generator to runback after the loss of the 21 MBFP. The main turbine has a non-safety related control circuit that automatically reduces the load on the turbine to a predefined level if the circuit senses plant power is greater than 85% and a MBFP is rotating at a rate of less than 3300 revolutions per minute (rpm). The purpose of this control circuit is to reduce the potential for a reactor trip due to a loss of a single MBFP. Because this circuit did not function, only the 22 MBFP, which is rated for about 60% power, was supplying feed water to the SGs. At the time, the SGs were producing 100% steam flow because the turbine runback circuitry did not function to runback and resulted in water levels decreasing in the four SGs. Control room operators inserted a manual reactor trip based on their conclusion they could not restore sufficient feed water to the SGs, or reduce the steam demand from the turbine, prior to an automatic reactor trip on low water level in the SGs.

Entergy personnel investigated the unexpected loss of the 21 MBFP and identified a stainless steel tube leak in the high pressure oil system associated with the 21 MBFP control system that caused reduced oil pressure below the MBFPs low oil pressure turbine trip setpoint. Entergy personnel determined the tube failed due to vibration induced metal fatigue. Entergy personnel performed extent of condition inspections on similar components in the 21 and 22 MBFP control oil systems. Entergy replaced the damaged tube and restored the system to service.

Entergy engineers and maintenance technicians initiated troubleshooting activities on the main turbine runback circuitry to determine the cause of the turbine runback failure during the transient. Entergy personnel were not able to identify a malfunctioning component in the runback circuitry. Entergy technicians tested the inputs to the system and tested the circuits operation including the MBFP turbine tachometer dropout relays and did not identify the malfunction experienced with the turbine runback circuitry. Station management implemented its decision making process and determined it was safe to startup the plant based on completed troubleshooting activities of this non safety-related circuitry in which operators are trained to respond to this scenario.

The inspectors performed system walkdowns, interviewed personnel, and reviewed design basis documents, troubleshooting plans, station procedures, and engineering evaluations.

b. Findings

The inspectors concluded that operators responded appropriately to the transient in accordance with their procedures and training. The inspectors also concluded that Entergys efforts at identifying the cause and extent of condition was adequate. Furthermore, the inspectors concluded that Entergys troubleshooting efforts to identify potential problems with the turbine runback circuitry were reasonable to demonstrate this function prior to plant restart. The following self-revealing finding was identified in relation to the installation of the MBFP hydraulic control system:

Introduction.

A self-revealing Green finding was identified because Entergy personnel did not establish adequate instructions in a design change package which resulted in incorrectly installed tubing in the 21 main boiler feed water pump (MBFP) hydraulic control system that subsequently failed due to fatigue.

Description.

On April 3, 2009, the 21 MBFP tripped off-line and steam generator water levels began to lower. The automatic main turbine runback circuitry did not actuate as designed to reduce main turbine steam demand. The control room operators attempted to manually reduce the main turbine steam demand but steam generator water inventory reduced to a level that required the operators to manually trip the reactor. Entergy personnel investigated the 21 MBFP trip and identified that a broken tube fitting resulted in high pressure control oil leaking to the oil sump and a subsequent trip of the 21 MBFP on low oil pressure.

Entergy staff sent the failed fitting to a vendor to be analyzed. The analysis determined the tubing likely failed from chronic cyclical stresses. Entergy personnel determined the tubing was installed incorrectly in 1986 when an engineering modification was implemented to upgrade the MBFP control system. Specifically, the stainless steel tubing was installed in a straight line with inadequate room to flex or expand, contrary to vendor installation instructions and existing maintenance procedures for installing tubing and Swagelok fittings.

The vendor and maintenance procedures required that tubing be installed with U shape bends to allow for expansion and flexing. Entergys root cause identified the engineering modification package used at the time of installation did not provide guidance on the tubing layout and did not provide specific instructions for tubing installation that were available in vendor manuals and site maintenance procedures. The root cause team confirmed that Swagelok installation manuals dating back to 1972 contained information on the proper use of gap gauges and examples of correct/incorrect tubing routing installations. The stations design change procedure required (section 5.3.11, Detailed Design Activities) that the design change package included specific installation and inspection requirements that are not addressed in existing installation specifications including known precautions and limitations.

Contrary to the design change procedure, specific instructions were not provided to ensure Swagelok fittings and tubing runs were installed in accordance with station procedures or vendor requirements including precautions to never run tubing in a straight run between rigid mounts. The inspectors determined it was reasonable for the station to provide correct guidance to the field installers in 1986 because the design change process required specific instructions to be provided and the design change packages were reviewed by multi-disciplined teams, including the maintenance department, who were cognizant of the standards for the installation of Swagelok fittings.

Entergy personnel inspected the MBFP control system tubing for the 21 and 22 MBFPs on Unit 2 and the 31 and 32 MBFPs on Unit 3. Entergy personnel identified a similar configuration on the 22 MBFP and replaced the tubing with the proper arrangement; the tubing on the Unit 3 MBFPs was found to be installed properly. Entergy personnel also developed corrective actions to evaluate training improvements for the installation or maintenance of tubing and compression fittings for site and supplemental personnel.

Entergy personnel plan to inspect and evaluate other compression fitting installations associated with other high speed rotating equipment.

Analysis.

The inspectors determined that a performance deficiency existed in that Entergy engineers did not provide adequate instructions to workers in order to install tubing in the MBFP control system in accordance with their design change program and vendor specifications.

The finding was more than minor because it was associated with the design control attribute of the Initiating Events cornerstone and affects its objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the incorrectly installed MBFP control tubing resulted in a loss of the 21 MBFP and, ultimately, a reactor trip due to low steam generator water level. In accordance with IMC 0609, Attachment 0609.04, Initial Screening and Characterization of Findings, the inspectors conducted a Phase 1 screening and determined this finding required a Phase 2 analysis because the finding contributed to both the likelihood of a reactor trip and the likelihood that the mitigation equipment functions will not be available (loss of redundancy in the feedwater system for other initiating events).

The inspectors determined the finding was of very low safety significance (Green) using the Phase 2 Indian Point Unit 2 Risk-Informed Inspection Notebook, in accordance with IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations. The inspectors determined that the exposure time was <3 days because the failure mechanism was a slow cyclic fatigue that resulted in failure only after the material had degraded to an unacceptable thickness and had demonstrated acceptable operation over the previous year while the MBFP was in operation. Using the <3 day exposure time, the inspectors solved: the Transient with Loss of Power Conversion System (TPCS) worksheet, increasing the likelihood of the initiating event by one order of magnitude, to address the increased likelihood of a reactor trip; and the Transients with Power Conversion System Available (TRANS) and Loss of Component Cooling Water (LOCCW) worksheets to address the loss of feedwater pump redundancy. This Phase 2 SDP estimated the increase in core damage frequency to be in the range of 1 in 50,000,000 years of reactor operation (low E-8 range). This range represents a finding of very low safety significance (Green). The dominant core damage sequence was a TPCS initiating event mitigated by the remaining ability to remove heat from the reactor core using auxiliary feed water or the primary bleed and feed functions.

The inspectors determined there was no cross-cutting aspect associated with the finding because the performance deficiency did not reflect current licensee performance.

Specifically, the performance deficiency occurred over 20 years ago and procedures have been improved in the design control, work control and vendor control processes since 1986 that reduce the likelihood of vendors working on equipment without the sufficient training or work instructions.

Enforcement.

Enforcement action does not apply because the performance deficiency did not involve a violation of a regulatory requirement, and the equipment involved is not safety related. Because this finding does not involve a violation of regulatory requirements and has very low safety significance, it is identified as FIN 05000247/2009003-01, Inadequate Design Change Package for Installation of Main Boiler Feed Pump Control System Tubing.

.2 (Closed) LER 2009-001-00, Technical Specification Prohibited Condition Due to a

Surveillance Requirement Not Previously Performed for the Atmospheric Steam Dump Valve Local Nitrogen Controls.

The inspectors reviewed Licensee Event Report (LER) 2009-001-00 dated April 27, 2009, to verify the LER was completed in accordance with 10 CFR 50.73 and that corrective actions identified were appropriate. The inspectors reviewed the circumstances of the January 2009 event and entries into the corrective action program including the apparent cause analysis.

The LER reported that a TS-required surveillance requirement (SR 3.3.4.2) was not previously performed for the nitrogen back-up supply to the steam generator atmospheric dump valves (ADVs). Specifically, Entergy personnel did not verify the nitrogen backup supply control circuit and transfer switch to the steam generator ADVs were capable of performing their intended function. Entergy personnel discovered this following testing of an engineering modification that installed an additional nitrogen supply for the atmospheric steam dump valves (ADVs) and determined that two of the four ADVs positioners were setup incorrectly. The equipment errors resulted in the failure of the valves to stroke open using the nitrogen backup supply; however, because of the design of the system, Entergy personnel determined the valves were able to stroke open using the normal station air supply. Because all four valves could operate using the station air system, and at least one ADV was operable using the nitrogen backup supply at all times in accordance with design requirements, the inspectors determined that no complete loss of ADV function had occurred. Entergy personnel repaired the positioners and established corrective actions to develop tests for the nitrogen backup supply and verified that the TS surveillance requirements have tests associated with them and are properly scheduled. Entergy documented the issues described above in CRs: IP2-2009-00062, -00069, -00077, -00137, and -00983.

The LER described a violation of TS 3.3.4, Remote Shutdown. The enforcement aspects of this finding are discussed in Section 4OA7. This LER is closed.

4OA5 Other Activities

Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that these activities were consistent with Entergy security procedures and applicable regulatory requirements. Although these observations did not constitute additional inspection samples, the inspections were considered an integral part of the normal, resident inspector plant status reviews during implementation of the baseline inspection program.

b. Findings

No findings of significance were identified.

4OA6 Meetings

Exit Meeting Summary

On July 22, 2009, the inspectors presented the inspection results to Mr. Joseph Pollock and other Entergy managers and staff, who acknowledged the inspection results. Entergy staff identified documents which were to be considered proprietary and handled as such.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy, for being dispositioned as a Non-Cited Violation.

  • Technical Specification Surveillance Requirement Not Previously Performed for Steam Generator Atmospheric Dump Valves

As described above in Section 4OA5.2, on January 7, 2009, following installation and post-work testing of an additional backup nitrogen supply to the ADVs, Entergy personnel identified that surveillance tests for the nitrogen backup supplies to the ADVs were never performed contrary to TS surveillance requirement 3.3.4.2.

The inspectors determined this constituted a violation of TS 3.3.4, Remote Shutdown, which includes the TS surveillance requirement to verify that the nitrogen backup supply control circuit and transfer switch to the steam generator ADVs are capable of performing their intended function. Contrary to this requirement, Entergy personnel did not verify the functionality of the control circuitry associated with the nitrogen backup supply to the ADVs.

The inspectors determined this issue was of very low safety significance (Green) per SDP Phase 1 screening because the safety function of the ADVs was not lost. Specifically, the inspectors determined the remote shutdown function for the steam generator requires only one ADV to be operable. All four ADVs were capable of being operated with the normal station air supply. Entergy personnel entered the issues into the corrective action program as CR-IP2-2009-00062, -00069, -00077, -00137, and -00983.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Entergy Personnel

J. Pollock, Site Vice President
A. Vitale, General Manager, Plant Operations
K. Davison, Assistant General Manager, Plant Operations
P. Conroy, Director of Nuclear Safety Assurance
B. Sullivan, Emergency Planning Manager
A. Williams, Site Operations Manager
S. Verrochi, System Engineering Manager
T. Orlando, Director, Engineering
R. Walpole, Licensing Manager
T. Cole, Project Manager

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000247/2009003-01 FIN

Inadequate Design Change Package

for Installation of Main Boiler Feed

Pump Control System Tubing

(Section 4OA3)

Closed

05000247/2009001-00

LER

Technical Specification Prohibited

Condition Due to a Surveillance

Requirement Never Performed for

the Atmospheric Steam Dump Valve

Local Nitrogen Controls (Section

4OA3)

LIST OF DOCUMENTS REVIEWED